&EPA United States Enviromental Protection Agency Office of Atmospheric and Indoor Air Programs EPA-430-R-94-011 June 1994 Energy-Efficient Refrigerator Prototype Test Results United Stales Office o! Atmospheric EPA-430-R-93-OC8 Emiromenlal Projection and Indoor Air June 1993 Agency Programs Multiple Pathways to Super-Efficient Refrigerators Uriled Slates Offico of Atmospheric EPAM30/R-92/OQ9 EfM/wnental Protection andlndoorAir Odober1992 Agency Programs S C P A Finite Element Analysis of Heat \S La r M Transfer Through the Gasket Region of Refrigerator / Freezer Recycled/Recyclable Printed with Soy/Canola Ink on paper that contains at least 50% recycled liber ------- ------- ACKNOWLEDGMENTS This report has been compiled by H. Alan Fine and Jean Lupinacci. of the Global Change Division of the U.S. Environmental Protection Agency and Professor Reinhard Radermacher of the Center for Environmental Energy Engineering at the University of Maryland. The authors wish to thank the many students at the University and technicians and engineers at the many companies who worked to develop the prototypes tested in this report. Particular thanks must go to Admiral Company, Frigidaire Company, GE Appliances, Haier Group, ShangLing Refrigerator Company, W.C. Wood Coppany Ltd., and Whirlpool Corporation for their donation of refrigerators and/or help in the manufacture of the prototypes. Many component suppliers, including Aladdin Industries, Inc., AMERICOLD, Degussa AG, Owens-Corning, and Thermalux, are also gratefully acknowledged for their donations and help on this project. ------- CONTENTS Page Findings 1 I. Introduction 3 LA. Purpose of Report 4 I.B. Energy Test Procedure 5 I.C. ERA Energy Calculations 7 II. Cabinet Modifications 9 II.A. Foam Insulation Enhancements 10 II.A.1. Thick-Wall Foam Insulation 10 II.A.2. Lower-Thermal Conductivity Foam Insulation—Carbon Black .... 12 ILB. Vacuum Insulation 14 II.B.l. VIP Insulation 15 ILB.l.a. VIP Insulation—Chest Freezers 15 II.B.l.b. VIP Insulation—Upright Freezers 17 II.B.l.c. VIP Insulation—Top-Freezer Refrigerators 18 II.B.l.d. VIP Insulation—Side-by-Side Refrigerators 20 II.B.2. Aerogel Insulation 22 ILB.3. Owens-Corning Evacuated Insulation 24 II.B.4. Aladdin Insulation 26 II.C. Improved Gaskets 27 II.C.l. Improved Gasket—VIP Insulated Refrigerator 28 III. Cycle Improvements 31 III.A. Improved Components 32 III.A.l. Linear Compressor 33 III.A.2. Inverter 34 III.A.3. Voltage Regulator 35 III.A.S.a. Green-Plug—New Top-Freezer Refrigerator 35 III.A.S.b. Green-Plug—Side-by-Side Refrigerator 36 III.A.4. Hot Water Refrigerator 37 III.B. Improved Refrigerants 38 III.B.l. Improved Refrigerants-Hydrocarbon Blends 38 III.B.2. Improved Refrigerators—Cyclopropane 39 III.B.3. Improved Refrigerators—HFC-134a and HFC-152a 40 III.B.4. Improved Refrigerants—HCFC-22 and HFC-152a Blends 41 11 ------- III.C. Improved Cycle . : 42 I III.C.1. Lorenz-Meutzner Cycle 42 IILC.l.a. Lorenz-Meutzner Cycle—Zeotropic Refrigerant Mixtures 42 III.C.l.b. Lorenz-Meutzner Cycle—Hydrocarbon Blends 43 III.C.l.c. Lorenz-Meutzner Cycle 45 ; III.C.2. Modified Lorenz-Meutzner Cycle 46 1 III.C.2.a. Modified Lorenz-Meutzner Cycle—U.S. Refrigerators ... 46 | III.C.2.b. Modified Lorenz-Meutzner Cycle—Chinese Refrigerator . 47 , III.C.3. Dual-Loop System . 48 III.C.4. Two-Stage Refrigerator 50 m.C.5. Kopko Cycle | 51 IV. System and Cabinet Modifications 59 ly.A. Double Insulation and Lorenz-Meutzner Cycle 60 I IV.A.1. Double Insulation 61 i IV.A.2. High-Efficiency Compressor 61 ; IV.A.3. Modified Lorenz-Meutzner Cycle 62 ! IV.A.4. Improved Gasket 63 I ly.B. Double Insulation and Kopko Cycle 64 i ! IV.C. Double Insulation and Alternate Refrigerants 67 IV.C.1. HFC-152a 67 i IV.C.2. Hydrocarbon Mixtures 68 V. References . 69 in ------- TABLES AND FIGURES Page TABLES I.I University of Maryland and Manufacturer Test Results 6 II. 1 Double-Insulated Refrigerators 11 II.2 Carbon-Black Foam Refrigerators 12 II.3 Typical Vacuum Insulation Thermal Conductivities 14 II.4 VIP Insulated Chest Freezers 15 II.5 VIP Insulated Upright Freezers 17 II.6 VIP Insulated Top-Freezer Refrigerators 18 II.7 VIP Insulated Side-by-Side Refrigerators 20 II.8 Aerogel Insulated Top-Freezer Refrigerators 22 II.9 OC Insulated Top-Freezer Refrigerators 24 11.10 Aladdin Insulated Top-Freezer Refrigerators 26 11.11 VIP Insulated Refrigerator with Improved Gasket 28 III.l Linear Compressor 32 III.2 Inverter 34 III.3 Green Plug—New Top-Freezer Refrigerator 35 III.4 Green Plug—Side-by-Side Refrigerator 36 III.5 Hot Water Refrigerator 37 III.6 Hydrocarbon Blends 7 38 III.7 Cyclopropane 39 III.8 Minimum Energy Consumption of the Optimized Systems 40 III.9 Calorimeter Data for the Two Compressors 40 111.10 HCFC-22 and HFC-152a Blends 41 III.ll Lorenz-Meutzner Cycle—Zeotropic Refrigerant Mixture 42 III. 12 Lorenz-Meutzner Cycle—Hydrocarbon Blends 43 III. 13 Lorenz-Meutzner Cycle 45 111.14 Modified Lorenz-Meutzner Cycle—U.S. Refrigerator 46 111.15 Modified Lorenz-Meutzner Cycle—Chinese Refrigerator 47 111.16 Dual Loop System 48 111.17 Two-Stage System 50 IH.18 Kopko Cycle 51 111.19 Kopko Cycle—First Modiacation 52 111.20 Kopko Cycle—First Modification Test Results 53 111.21 Kopko Cycle—Second Modification 54 111.22 Kopko Cycle—Second Modification Test Results 55 111.23 Kopko Cycle—Third Modification and Test Results 56 111.24 Kopko Cycle—Fourth Modification and Test Results 57 IV ------- I V.I Double-Insulated, Lorenz-Cycle Refrigerator IV.2 High-Efficiency Compressor IV.3 Modified Lorenz-Meutzner Cycle IV.4 Double-Insulated, Kopko-Cycle Refrigerator IV.5 Specifications for the First Modification IV.6 Test Result for the First Modification IV. 7 Compressor Comparison for Kopko Modifications . IV.8 Increased Insulation with Refrigerant HFC-152a . . . IV.9 Increased Insulation with Hydrocarbon Refrigerants 60 61 62 64 65 66 66 67 68 FIGURES 11.1 Cross Section of Gasket Region II.2 Front View of Gasket Region . . 29 30 I V.I Schematic Representation of Improved Gasket 63 ------- VI ------- Prototype Test, Results May 1994 FINDINGS Working prototype refrigerator/freezers demonstrating a wide variety of existing and emerging technologies for energy conservation have been built and tested. Energy-efficiency gains resulting from improvements to individual components can be grouped as follows: n o Energy Reduction 5-10 10-15 15-20 25-30 , Improvement improved gasket region design inverter hydrocarbon refrigerants 50% coverage advanced insulation linear compressor Lorenz cycle in side-by-side R/F Lorenz cycle in top-freezer R/F Kopko Cycle Adding 1.5 inches of foam insulation Substantial energy-efficiency gains resulting from a combination of improvements can be grouped as follows: % Energy Reduction 30-40 40-50 >50 Improvements Adding 1.5 inches of insulation and Kopko cycle Adding 1.5 inches of insulation, better compressor, Lorenz cycle, and improved gasket Adding insulation, better compressor, and HFC-152a refrigerant to a Chinese R/F Adding insulation, better compressor, and hydrocarbon refrigerants to a Chinese R/F The EPA Refrigerator Analysis (ERA) model predictions agree with measurements made on the prototypes. ------- Energy-Efficient Refrigerators ------- Prototype Test Results May 1994 I. INTRODUCTION Many factors have driven industry to implement energy-efficiency improvements in household refrigerator/freezers (R/Fs). The 1993 DOE Energy Efficiency Standards have been in effect for a little more than one year, and many manufacturers have models on the market that exceed this standard. In fact, the winner of The Golden Carrot Competition for $30 million, Whirlpool Corporation, will be selling R/Fs in 1994 that exceed the standard by more than 25 percent, without using ozone-depleting CFCs. Other manufacturers are expected to offer similar energy efficient products in the near future. There appears to be dramatic changes occurring in consumer buying preferences. Consumer acceptability is an important factor to selling refrigerators. Based on the marketing perception that consumers are only first cost driven and place high value on internal volume, manufacturers were reluctant to explore cost-effective design changes to increase energy efficiency, particularly by adding more insulation to the refrigerator walls. The recent success of Sears's program to prominently market the "Energy Efficient" 1993 moldels may change the idea that energy efficiency would not drive the sale of refrigerators. The Sears program consisted of training, advertising, point-of-sale identification, and charts that helped customers understand the substantial savings and environmental benefits from purchasing energy-efficient refrigerators. Early indications from Sears showed that many customers would ask for the new models and were even willing to wait and pay more for them. There is not just one path or design approach that leads to super-efficient refrigerators but rather multiple pathways to achieve large energy savings. Each refrigerator manufacturer will decide on the most cost-effective set of options emd technologies based on tits current products' energy efficiency, design, size class, cost-structure, and other factors. In evaluating the potential energy savings in R/Fs, EPA has conducted a wide variety of analyses, including technical evaluations, model development and analysis, cost analyses, marketing and consumer preference analysis, and prototype development and testing. All are necessary to determine the ultimate acceptability of the various options. Manufacturers will conduct similar analyses pertaining to their own product lines and circumstances as they commercialize new energy-efficient products. ------- Energy-Efficient Refrigerators LA PURPOSE OF REPORT This report will summarize the test results for the numerous R/Fs built by EPA and our partners to evaluate a wide variety of technologies to increase energy efficiency and to eliminate the use of CFCs. The results for many of the prototypes represent the joint efforts of EPA, the University of Maryland, and various equipment and refrigerator manufacturers. In many cases, the prototypes were tested at both the University and the individual companies. The partnerships were a critical component of the success of the prototypes. The interaction between the various experts was useful to define realistic parameters, resolve problems, and make modifications to the prototypes on the production line. The prototypes were developed to test technologies that increase energy efficiency and eliminate CFCs. The refrigerators that were built and tested are not meant to showcase all combinations of technologies, but rather to demonstrate significant energy savings that could be achieved with existing and emerging technologies. Some of the prototypes were built to test the performance of a single technology. Other prototypes combined technologies that demonstrated substantial energy savings to identify any interactive effects between the different technologies and different systems. The report is divided into four sections. • The Introduction describes the purpose of the report, the testing methodology, and comparison with ERA energy calculations. • The Cabinet Improvements section summarizes the test results from refrigerator/ freezers that demonstrate improvements to the thermal envelope of the unit. • The Cycle Improvements section summarizes the test results from refrigerator/freezers that demonstrate improved components, alternate refrigerants, and alternate cycles. • The System and Cabinet Modifications section provides a summary of test results from units that combined both improvements to the cycle and the cabinet. Many technologies have shown great promise for future development, but further evaluation will need to be conducted for commercialization. Continued applied research, manufacturability, long-term reliability, and cost analyses may be required by the manufacturers. ------- Prototype Test Results May 1994 I.B ENERGY TEST PROCEDURE Except as noted, refrigerator energy tests were performed at the University of Maryland (Ul Md.) according to the DOE test procedure, with some minor modifications. The modifications were necessary to arrive at well optimized refrigeration cycles in a short period of time. For those tests that included a defrost cycle and the anti-sweat heaters, the outcome is the same as for the DOE procedure. During testing at U. Md., all compartment temperatures and the room temperature are measured and maintained as prescribed by DOE. The compartment temperatures, however, are maintained with an independent temperature controller, not the original refrigerator thermostat. Generally, the temperature controller controls the freezer temperature, while the food compartment temperature is adjusted by either a second controller (Kopko and dual loop systems) or by adjusting charge and capillary tube length. The instantaneous power and energy consumption are measured with watt and watt-hour transducers, respectively. i The defrost is normally deactivated during testing at U. Md. and tests are conducted for one day (24h). The system, however, is defrosted regularly to maintain system performance. When a defrost cycle is included in the measurement at U. Md., the energy consumption is measured from the onset of one defrost cycle to the onset of the next. The energy consumption is then extrapolated to 24h. When defrost cycles and anti-sweat heaters in the on and off positions are included, the U. Md. method is the same as the DOE method, except it is faster and more accurate. The refrigerator performance is determined at a freezer temperature of 5°F rather than measuring above and below this temperature and then interpolating to it. Modifications to the defrost cycle were not tested. In certain instances, such as the incorporation of either the Lorenz or Kopko cycle into the R/F, additional energy savings could be achieved by modifying the defrost cycle. Table LI reports refrigerator tests that were repeatable within ±1 percent when repeated under the same conditions and at the same laboratory, and within +. 5 percent when compared to other laboratories. The table also shows a comparison of the U. Md. test results and the test results of the manufacturers conducted according to the DOE standard. ------- Energy-Efficient Refrigerators Table I.I University of Maryland and Manufacturer Test Results : : . -• Energy ! Test Location land FF Temperature I|Z Temperature Consumption ; ModeJ Tested Conditions • (°F) . (°F) (kWh/24h) ; t ; • i Admiral RB19xx with vacuum insulation Whirlpool ET20ZK Thick-wall 20 ft3 Whirlpool U. Md. w/o defrost U. Md. with defrost Admiral DOE Test U. Md. with anti-sweat heaters on Whirlpool with anti- sweat heaters on U. Md. with anti-sweat heaters on Whirlpool with anti- sweat heaters on U. Md. with anti-sweat heaters off Whirlpool with anti- sweat heaters off 5.3 4.9 5 5.0 5.0 5.0 5.0 5.0 5.0 38.5 38.3 38 41.9 40.0 37.4 38.1 37.1 36.6 1.96 2.16 2.12 2.17 2.31 1.91 1.85 1.38 1.44 ------- Prototype Test Results May 1994 I.C ERA ENERGY CALCULATIONS The EPA Refrigerator Analysis (ERA) computer model can be used to estimate the impact on energy consumption of a wide variety of modifications to the refrigerator cabinet and components. ERA predicts the performance (energy consumption) of household R/Fs and is capable of simulating various cabinet, auxiliary, and cycle configurations. It consists of four major components: 1. j^. menu-driven input processor; 2. Estimation of the cabinet loads; 3. Thermodynamic cycle simulation; and i 4. Energy-consumption calculations. I ; Additional details are provided in the ERA User's Manual. [1] The results of a variety of ERA calculations have been presented in. Multiple Pathways to Super-Efficient Refrigerators. [2] These results have been compared to the test results of applicable prototype models. ------- Energy-Efficient Refrigerators 8 ------- Prototype Test Results May 1994 II. i CABINET MODIFICATIONS A series of prototype refrigerator/freezers (R/Fs) were produced that contained improvements to the thermal envelope of the units. These improvements included: • Improvements to the foam insulation system, • The addition of vacuum insulation, and/or i • Improvements to the gasket system. l Details of the prototypes and the resulting energy savings are presented in the following section. ------- Energy-Efficient Refrigerators II.A FOAM INSULATION ENHANCEMENTS The overall thermal performance of the cabinets was improved by increasing the thickness of the R/F cabinet or by reducing the thermal conductivity of the foam., The results of these tests are described next. ••>•., II.A.1 Thick-Wall Foam Insulation Polyurethane foam insulation was added to the walls of a refrigerator to reduce heat: flow into the refrigerated volume. The internal volume was maintained by adding the insulation to the exterior of the. unit, at the expense of slightly larger exterior dimensions. Alternatively, insulation can be added to the interior surfaces, but at the expense of internal volume. Baseline Unit The baseline unit was a standard 20 ft3 automatic-defrost top-freezer refrigerator, Whirlpool model number ET20DK. Dimensions and daily energy consumption are presented in Table 11.1. Thick-Wall Unit The "double-insulated" refrigerator was manufactured by installing the liner for the" standard 20 ft3 model into the shell of a standard 25 ft3 unit, model ET25DK. The unit was then foamed and completed with components identical to those for the standard ET20DK. Special doors did, however, have to be manufactured to fit the unit. Two units were built and tested at Whirlpool. 10 ------- Prototype Test Results May 1994 Table H.l Double-Insulated Refrigerators Baseline Thick- Wall Unit Unit Volume (ft3) Freezer Fresh Food Exterior Dimensions (in) Height Width Depth Insulation Thickness (in) Doors FF Sides FF Back FF Bottom FZ Sides FZBack FZTop Mullion Energy Consumption Whirlpool (kWh/24h) U.Md. EPA-RTP 5.5 14.4 66 32 28 1.5 1.8 1.8 1.8 •2.2 2.2 2.2 2.5 2.33 5.5 14.4 69 35 31 2.8 3.3 3.6 3.3 3.6 4.0 3.6 2.5 1.63 + 0.03 1.73 1.72 Discussion As can be seen from the above table, approximately 1.5 inches of foam • were added to all exterior surfaces of trie unit. Interior volume was i maintained, while exterior dimensions were increased by 3 inches on each i dimension. A measured 27 percent decrease in energy consumption was achieved. The ERA model predicts a 19 percent energy reduction for the addition of 1 inch of insulation to the exterior of 18 ft3 R/Fs and 29 percent for the addition of 2 inches. ,[2] ERA is thus in good agreement with the measurements. 11 ------- Energy-Efficient Refrigerators II.A.2 Lower Thermal Conductivity Foam Insulation—Carbon Black The thermal performance of foam insulation is a complex function of three modes of heat transfer that occur within the insulation: heat conduction in the solid and vapor phases and thermal radiation through the composite. Reducing the amount of heat transferred by any of these mechanisms should reduce the thermal conductivity of the foam and the rate of heat flow through the foam for a given set of conditions. The addition of carbon black particles to polyurethane foam reduces thermal radiation transport and the thermal conductivity of the foam. Black foams have been developed for the construction industry and are under development for appliance applications by Miles Inc. and the Center for Applied Energy Research Inc. [3] Baseline Unit Black-Foam Units The baseline model was a standard 17 ft3 automatic-defrost top-freezer model, Admiral Co. model number RB17OPW. Foaming of pre- assembled empty cabinets with an HCFC-141b-blown foam was done at Miles Inc. The foam formulation was developed by Miles for this trial. After foaming, the units were returned to Admiral for final build-up and testing. Foam properties and energy test results are shown in Table 11.2. [3] Foam with the same formulation but containing 6.3 percent carbon black was used for these units. All other processing and testing protocols were identical. Table IL.1 Carbon-Black Foam Refrigerators i ' i ' 1 Baseline Black-Foam " ' ; Units ! Units . • : ; : -:1 " • : -. , - -r ! r Foam Thermal Conductivity (BTU*in/(h*ft?*0F)) Foam Density (Ib/ft3) Energy Consumption (kWh/24h) 0.129 1.75 1.84 + 0.03 0.12 1.87 1.83 + 0.01 Discussion The thermal conductivity of the carbon-black loaded foam was eight percent lower than the baseline HCFC-141b foam. Computer model simulations made by Admiral predicted a 3.2 percent lower energy consumption for the refrigerator. ERA predictions for 18 ft3 models [2] show energy reductions ranging from 3.4 to 4.3 percent with an average of 4.0 percent. 12 ------- Prototype Test Results May 1994 The actual energy consumption of the black-foam prototype refrigerator was less than one percent lower than the baseline. Tests, including reverse heat flow measurements, are being performed to determine why larger energy savings were not observed. One hypothesis for why the eight percent lower thermal conductivity black-foam did not reduce the energy consumption of the unit was that the black-foam units were made in February 1993 and the baseline models in May. Small improvements in components over this period may have lowered the energy consumption of the baseline models and masked the effect of the improved foam. 13 ------- Energy-Efficient Refrigerators II.B VACUUM INSULATION A number of advanced insulation systems are currently under development. These systems generally consist of a filler material contained in a gas-tight barrier. All of the concepts, except for gas-filled panels, attain their lower thermal conductivity at reduced pressure (under vacuum). Filler materials incorporated into these advanced insulations include ceramic spacers, precipitated silica or other powders, fiberglass, aerogel tiles, and open-cell foams. Barrier materials range from laminated polymer structures to stainless steel. High thermal resistance (low thermal conductivity) elements can be combined with foam insulation in the walls of R/Fs to improve their thermal performance, without effecting their structural integrity. Four types of advanced insulation systems were tested in R/Fs and/or freezers. Typical center-of-panel properties for the vacuum insulations employed in the prototypes are summarized in Table II.3. It is important to note that the conductivities of panels used in the prototypes may be substantially higher than those given in the table, as edge effects may substantially change the thermal performance of small panels, especially those fabricated with metallic barriers. Table II.3 Typical Vacuum Insulation Thermal Conductivities * 1 ; :' 1 ' : ; ' ; : ! Thermal Conductivity ; Description \ ' Manufacturer (BTU*in/(h*ft2*°F)) 1 • • i . - i Precipitated Silica in Plastic Laminate (VIPs) Aerogel Tiles in Plastic Laminate Fiberglass in Stainless Steel Precipitated Silica and Carbon Black in Stainless Steel Degussa AG Thermalux Owens-Corning Aladdin Industries, Inc. 0.050 ±0.0031 0.051+ 0.0011 0.018 + 0.0022 0.0421 Measurements made by Materials Thermal Analyses Group at Oak Ridge National Laboratory. 1 Measurements made by Owens-Corning. 14 ------- Prototype Test Results May 1994 II.B.1. VIP Insulation j WB.l.a VIP Insulation—Chest Freezers Vacuum insulation panels (VIPs) consisting of precipitated silica filler in a plastic- laminate barrier/container were installed in three chest freezers at W. C. Wood Co. Ltd. injNovember 1991. The balance of the composite insulation system consisted of W. C. Wood's standard foam formulation blown with CFC-11. Baseline Units Two production model chest freezers were employed as baseline units: i WC42-xx and WE46-xx. Storage capacity, insulation thickness, and ; energy consumption data for these models are listed in Table II.4. \ VIP Units VIPs were mounted on styrofoam inserts adjacent to the cold-wall I evaporators on the sides and bottom of the three prototype units. The i cabinets were then assembled, foamed, and built-up on the production } line without any additional modifications. The percentages of area i covered by VIPs and energy consumption results are presented in the j following table. Additional details on panel sizes and locations are i available in reference [4]. i ' I i Table HA VIP Insulated Chest Freezers WC42-XX • ; . ' ; ; #1 Capacity (ft3) Insulation Thickness (in) Baseline Energy Consumption (kWh/24h) % Area Covered by VIPs Energy Consumption (kWh/24h) % Energy Reduction 14.8 2.5 1.16 54 1.04 11 WC42-Jx ; WE46-XX •U.1 14.8 2.5 1.16 54 0.99 15 16.5 3.0 1.24 44 1.08 13 Discussion An average 13 percent reduction in energy consumption for an average I 50 percent area of coverage was obtained. The baseline models were i relatively high-efficiency models incorporating thick insulation walls. j The impact of VIPs on energy consumption would thus be less than that 1 for freezers or R/Fs with thinner walls. 15 ------- Energy-Efficient Refrigerators Measurements performed, on the WC42-xx units approximately 18 months after production showed 13 and 16 percent increases in energy consumption with 12 and. 7 percent increases in run time for units 1 and 2, respectively. The increase for unit one is much higher than that which would be expected from the aging of the foam alone. Either a panel failure or aging of the panels must have occurred. The increase in run time for unit two would be consistent with foam aging. The significant increase in energy consumption, as compared to the increase in run time, has not been explained. 16 ------- Prototype Test Results May 1994 II.B.l.b VIP Insulation—Upright Freezers VIPs were installed in upright freezers at W. G. Wood Co. Ltd. in February 1992. The balance of the composite insulation system consisted of W. C. Wood's standard CFC-11 blown foam insulation formulation, with the exception of fiberglass doors. Baseline Units Two production model upright freezers were used as baseline models: WVF47-xx and WV58-xx, Data on these models are presented in Table 71.5. Vllf Units VIPs were mounted on the sides, back, and top of the smaller unit and ! on the sides, back, top, and bottom, of the larger model. Cabinets were I then assembled, foamed, and built-up on the production line without j any other modifications. Percentages of area covered and test results follow. Additional details on panel sizes and locations can be found in reference [4]. Table IL5 VIP Insulated Upright Freezers _ • . " ' : : . WVF47-XX . WV58-xx Capacity (ft3) Insulation Thickness, (in) Baseline Energy Consumption (kWh/24h) % Area Covered by VIPs Energy Consumption (kWh/24h) % Energy Reduction 16.7 2.5 2.15 , 56 ' 2.02 6 20.3 2 •2.34 ,-=.-: 53 . 2.05 12 Discussion The approximately 10 percent energy reduction is lower than that achieved for the chest freezers even though the walls are thinner. This probably results from the fiberglass insulated door, which allow a disproportionate amount of heat to flow into the cabinet. Retests on the prototypes performed approximately 14 months after production showed a 5 percent increase in energy consumption and compressor run time. This is consistent with aging of the foam insulation, alone/over this period. 17 ------- Energy-Efficient Refrigerators IJ.B.2.C VIP Insulation—Top-Freezer Refrigerators VIPs were installed in 19 ft3 automatic-defrost top-freezer refrigerators produced by the Admiral Company in 1991 and 1992. The balance of the insulation system was either Admiral's standard foam formulation blown with CFC-11 or a special CO2-blown formulation. Baseline Units The 1991 baseline units were standard Model RB19xx production units built during the last quarter of the year. The 1992 baseline models were RB19K2A production models, modified with a flat back to accommodate larger VIPs. Foam insulated doors also replaced the standard fiberglass insulation in all baseline models. DOE energy test results for the various units are presented in Table 11.6. VIP Units VIPs were mounted on the sides and top adjacent to the steel cabinet and on the back adjacent to the plastic liner on all prototype units. Panels were also mounted adjacent to the steel cabinet bottom on the 1992 units. Cabinets were then assembled, foamed, and built-up without any additional modifications. Three sets of cabinets and doors were generally produced. These components were tested together or in combination with doors or cabinets from the baseline models to generate the data presented below. Additional information on the panel sizes and locations can be found in references [5] and [6}. Table 11.6 VIP Insulated Top-Freezer Refrigerators \ : ! ' - " 1 : : -1 ..---. Year ; 1991 j 1992 1992 Foam Blowing Agent Baseline DOE Energy Consumption (kWh/24h) VIPs in Cabinet and Doors % Area DOE Energy % Reduction VIPS in Cabinet only DOE Energy % Reduction VIPs in Doors Only DOE Energy % Reduction CFC-11 2.36 + 0.12 47 2.12 + 0.05 10 2.27 + 0.06 4 2.23 + 0.07 5 CFC-11 2.26 + 0.06 68 2.08 + 0.06 8 2.15 + 0.06 5 2.21 + 0.01 2 C02 2.58 + 0.10 68 2.26 + 0.09 13 18 ------- Prototype Test Results May 1994 Discussion The energy reduction results for the 1992 prototypes were less than i expected. The results for the units made with CFC-11 foam are based on only two sets of cabinets and doors. Two additional sets were made | but found to have very poor energy performance. These units were I disassembled after testing and found to have punctured panels. The i percentage reduction for the poorer insulating CO2-blown foam was as ' expected. Measurements were not made for the cabinet-only and door- 1 only configurations, as rapid aging of these foams would have produced ' confusing results. I The average 10 percent energy reduction is smaller than the 14 to 16 percent predicted by ERA for 50 percent area of coverage of several ! 18 ft3 refrigerators. [2] The ERA calculations were based on 1-inch thick ' panels, while the tests were performed with 0.5- and 0.75-inch thick ' panels. Linear extrapolation of the test results for the 1991 prototypes to 1-inch thick panels yields a 14 percent energy reduction. Similar i calculations for the 1992 prototypes yields 12 and 19 percent reductions for the CFC-11 and CO2 foams, respectively. Only the results for the i 1992 prototypes with CFC-11 foam are not in good agreement with ERA. As mentioned previously, there may have been problems with ; punctured panels in these tests. 19 ------- Energy-Efficient Refrigerators ILB.l.d VIP Insulation—Side-by-Side Refrigerators A set of 22 ft3 side-by-side refrigerators were built at Admiral Co. in 1991. The insulation system in these units consisted of VIPs and Admiral's standard CFC-11 foam formulation. Baseline Units The baseline units were standard production models built in late 1991, model CNS22V8A. All walls and doors of the baseline units contained foam insulation. VIP Units VIPs were mounted on the top, sides, and doors of the prototype units. All panels were attached to the steel case, except the back panels that were attached to the liner. Cabinets were then assembled, foamed, and completed without any additional modifications on the production line. Additional details on panel sizes and location can be found in reference [5]. Test data are presented in the following table. Table IL7 VIP Insulated Side-by-Side Refrigerators Baseline DOE Energy Consumption (kWh/24h) 2.98 + 0.08 VIPs in Cabinet and Doors % Area Covered by VIPs DOE Energy % Energy Reduction 49 2.96 ± 0.07 1 VIPS in Cabinet only DOE Energy % Energy Reduction 2.82 ± 0.07 5 VIPs in Doors Only DOE Energy % Energy Reduction 3.06 + 0.15 -3 Discussion The presence of the VIPs in the long slender doors of the side-by-side units resulted in warpage and poor sealing. Thus the energy consumption went up for the doors-only case and only went down one percent for the cabinet and doors case. Foam voids were also observed in the cabinet. These were patched prior to energy testing but may have contributed to the small reduction in energy that resulted for the cabinet-only tests. 20 ------- Prototype Test Results May 1994 Similar vacuum panels at approximately 55 percent area of coverage have been installed in a 25 ft3 side-by-side model. [7] These panels resulted in a 17 percent reduction in energy consumption. 21 ------- Energy-Efficient Refrigerators II.6.2 Aerogel Insulation Panels consisting of aerogel tiles encapsulated in a plastic laminate barrier/container were installed in top-freezer automatic-defrost refrigerators. The panels were manufactured by Thermalux from 12 in. by 12 in. by 0.5 in. silica aerogel tiles, which were cut and assembled into the desired panel sizes. The refrigerators were made at Admiral Co., and the remainder of the insulation composite was their standard foam formulation blown with CFC-11. Baseline Units The baseline units were standard Admiral production models manufactured in 1992, model RB19K2A. Several indentations in the backs of the units were eliminated to allow a higher coverage of vacuum panels. Foam-insulated doors were also used to replace the standard fiberglass insulation. All other dimensions and components were unchanged from the standard production models. Aerogel Units Three prototype units containing aerogel panels were fabricated. Aerogel panels were attached to all surfaces of the prototypes, including the bottom. All panels except those on the back were attached to the steel case. The panels were 1-inch thick, except those on the fresh food compartment sides, bottom, and back, which were 0.5 inches thick. The units were assembled, foamed, and completed on the normal production line without any additional modifications. Additional details on panel sizes and locations can be found in reference [6]. Test results follow. Table II.8 Aerogel Insulated Top-Freezer Refrigerators Baseline DOE Energy Consumption (kWh/24h) Panels in Cabinet and Doors % Area Covered by Aerogel DOE Energy % Energy Reduction Panels in Cabinet only DOE Energy % Energy Reduction Panels in Doors Only DOE Energy % Energy Reduction 2.26 + 0.06 67 2.10 + 0.09 7 2.12 + 0.07 6 2.24 + 0.05 1 22 ------- Prototype Test Results May 1994 Discussion The aerogel panels were very fragile, and several were broken during i shipment. After energy testing, one prototype was disassembled and ! also found to have panels that had lost their vacuum. The panels j located on the bottom of the units also blocked foam flow, resulting in ; voids that had to be patched. These two problems account for the poor performance of these prototypes. | Additional tests of this insulation are not currently possible, as • Thermalux has gone out of business, and they were the only known ; supplier of large aerogel tiles. 23 ------- Energy-Efficient Refrigerators II.B.3 Owens-Corning Evacuated Insulation Vacuum panels consisting of fiberglass in a stainless steel container are produced by Owens-Corning (OC). As noted earlier, these panels may have center-of-panels thermal resistivities higher than 50 h*ft2*°F/(BTU*in), but edge effects may substantially lower their performance in refrigerators. Baseline Units Baseline units were 1992 Admiral RB19K2A models with flat backs and foamed doors as described in section II.B.l.c. OC Units Four prototypes were built with OC panels. Panels were 0.75 inches thick, except for the fresh food back, which was 0.5 inches thick. Small panels were used in two of the prototypes to cover the machine compartment. All four units had panels on the other five sides. After mounting the panels, the cabinets were assembled, foamed with Admiral's standard CFC-11 foam formulation, and completed on the production line. Test results follow. Table II.9 OC Insulated Top-Freezer Refrigerators Baseline DOE Energy Consumption (kWh/24h) Panels in Cabinet and Doors % Area Covered DOE Energy % Energy Reduction Panels in Cabinet only DOE Energy % Energy Reduction Panels in Doors Only DOE Energy % Energy Reduction 2.26 + 0.06 69 1.92 + 0.05 15 1.99 + 0.05 12 2.18 ± 0.04 4 Discussion The energy reduction results were the best of the advanced insulations tested. This is probably reflective of the higher thermal resistances of the panels, measured by Owens-Corning to average almost R-40 per inch including edge effects. The two units with panels over the machine compartments did not have significantly different energy consumption than those without these 24 ------- Prototype Test Results May 1994 panels. This is indicative of the fact that small panels will not have an improved performance over foam, especially for panels with metallic edges. , One unit was also known to have a panel that had lost its vacuum. Again, the performance was not significantly different than that of the other units. This is probably indicative of the small number of prototypes and the variability in the other components of the refrigerator masking the effect of one bad panel. 25 ------- Energy-Efficient Refrigerators II.B.4 Aladdin Insulation Evacuated panels containing a blend of precipitated silica and carbon black contained in stainless steel are produced by Aladdin Industries. These panels have slightly higher center-of-panel thermal resistance than the panels contained in plastic, but edge effects may substantially lower their effectiveness. Baseline Units The baseline models were 1993 RB193PW refrigerators produced by Admiral. The only modification to the standard units was the use of 2-inch thick doors. At the request of Admiral, only percentage changes from the baseline are presented in this report. Aladdin Units Three prototype units were built with Aladdin panels. All panels were 1-inch thick, except for 0.5 in. panels on the fresh food back. Panels were not placed over the machine compartment. Except for the panels and 2-inch thick doors, the prototypes were identical to standard production models. Foam blown with CFC-11 was used for the balance of the insulation system. [6] Table 11.10 Aladdin Insulated Top-Freezer Refrigerators Baseline DOE Energy Consumption Panels in Cabinet and Doors % Area Covered % Energy Reduction Panels in Cabinet only % Energy Reduction 100% 57 6 5 Discussion The Aladdin panels had approximately 15 percent higher areas of coverage and 25 percent higher center-of-panel thermal resistances than the panels contained in plastic. The energy reductions were, however, lower. Edge effects are clearly very important. Higher center-of-panel thermal resistances and larger panels can overcome this problem, as demonstrated by the Owens-Corning insulation results. 26 ------- Prototype Test Results May 1994 ILC Improved Gaskets Heat flow through the gasket region of the cabinet contributes significantly to the total load. Finite element analysis (PEA) of this region of the refrigerator cabinet has shown that heat flow in this region can be reduced by 50 percent by minor changes to the design of the flanges on the door and cabinet. [8] Test results for two prototype units with gasket modifications are presented in the next section and section IV.A. 27 ------- Energy-Efficient Refrigerators II.C.1 Improved Gasket—VIP Insulated Refrigerator Heat flow in the gasket region occurs by conduction down the flanges and then by convection from the ends of the flanges and the gasket. Replacing a portion of the flanges on the inside of the refrigerator with plastic can reduce the total amount of heat flow in this region by one-half. In many cases, the cabinet flange does not extend into the cabinet as far as the gasket. Unless the small gap between the gasket and interior liner is sealed, convection from the end of the flange will still occur as if the flange extended into the refrigerated volume. Baseline Unit One of the Admiral RG19xx prototype units built in 1991 and containing VIPs was used in this test program (see II.B.l.c.). The energy tests were performed at U. Md. with the anti-sweet heaters off (one portion of the standard DOE test). Modified Unit A cross section of the gasket region is shown in Figure ILL The cabinet flange was modified by adding a piece of foam insulating tape adjacent to the flange on the inside of the refrigerated volume. The door flange was modified by removing the metal that protruded through the flange region. A front view of these modifications is shown in Figure 11.2. Table 11.11 VIP Insulated Refrigerator with Improved Gasket Baseline Energy Consumption (kWh/24h) Energy consumption with door flange modification % Reduction Energy consumption with both flanges modified % Reduction 2.18 + 0.02 2.11 3 2.01 + 0.01 8 Discussion Slightly greater energy reductions could be achieved by redesigning the door flange, as opposed to removing the flange from between the screw holes. ERA predicted energy reduction of 7 and 11 percent for 25 percent and 50 percent reductions in heat flow through the gasket region, respectively. The FEA results indicate that an approximately 40 percent reduction in heat flow should have occurred, with the modifications performed. Thus agreement between ERA and the test results is very good. 28 ------- Prototype Test Results May 1994 Figure II.l Cross Section of Gasket Region Door Door Flange Foam Insulation Cabinet Flange Gasket Removal Metal Insulating Tape Foam Inner 29 ------- Energy-Efficient Refrigerators Figure 11.2 Front View of Gasket Region | 3: HI I la 0> T3 US 55 CO O o o K ,,9'se . 55 1 '£ *a O 30 ------- Prototype Test Results May 1994 III. Cycle Improvements t i Aj series of prototype refrigerators was also produced with improved cycle components. Improvements included: • i Improved components, i • Alternate refrigerants, and i • j Alternate cycles. The results of tests on these prototypes are presented in this section. 31 ------- Energy-Efficient Refrigerators III.A. IMPROVED COMPONENTS III.A.l Linear Compressor A linear compressor differs from a conventional reciprocating compressor in that the motor drives the piston directly. This feature eliminates the crank mechanism and simplifies the design. In the linear compressor developed by SunPower Inc., gas bearings guide the piston as it resonates on a spring. Use of gas bearings and elimination of the crank greatly reduces friction losses and eliminates the need for lubricating oil. The resonant piston reduces motor size and improves motor efficiency. Reducing the input voltage to the linear motor reduces the stroke of the piston and allows for easy capacity control. The net result of these improvements is a simple, efficient, oil-free, variable-capacity design. Compressor calorimeter tests with the SunPower compressor have shown a 15 percent improvement in design efficiency compared to a conventional reciprocating design. [9] Baseline Unit The baseline unit was an 18.6 ft3 top-freezer automatic-defrost refrigerator produced by Frigidaire, model number FPGS19TSWO. Prototype Unit The compressor was replaced with the linear compressor. The capillary tube and refrigerant charge were optimized for minimum energy consumption. Thermocouples were installed. The remainder of the baseline unit remained unchanged. Table 111.1 Linear Compressor ••..'<:• .1 • . 1- T. • • .!. :i ; Linear . \ Baseline , Compressor 1 • ! I1' r . ! " Compressor EER Charge (g) Energy Consumption (kWh/24h) FF/FZ Temperature (°F) Duty Cycle % Energy Reduction 5.5 156 1.94 45.2/4.6 0.52 6.2 200 1.73 46.1/4.4 0.48 11 32 ------- Prototype Test Results May 1994 Discussion The linear compressor was more efficient than the original compressor and produced an 11 percent energy savings. The savings were smaller than expected when compared on an HER basis because the fans also consume electricity. ERA predicted a 10 percent energy savings when the linear compressor replaced a 6.0 EER reciprocating compressor in an 18 ft3 R/F. [2] The linear compressor in the ERA analysis was assumed to have an EER of 6.5 and variable capacity control. The test did not include capacity control, and the linear compressor had an EER of 6.2 and replaced the Frigidaire unit, which had a 5.5 EER. 33 ------- Energy-Efficient Refrigerators III.A.2 Inverter An inverter is a variable-frequency power source that can be used to vary the speed of electric motors. The inverter used in the experiments is a proprietary design. It works with conventional permanent split capacitor (psc) motors such as those used in refrigerator compressors. Baseline Unit The baseline unit was an 18 ft3 top-freezer automatic-defrost refrigerator manufactured by Whirlpool. Prototype Unit A 90 V inverter was added to the power supply to the compressor. The fan voltage and frequency was not changed. Table III.2 Inverter — . _ _ . — . — . ,— : 1 : Baseline Inverter FF/FZ Temperature (°F) Energy Consumption (kWh/24h) Duty Cycle % Energy Reduction 42.3/4.4 2.49 0.57 42.3/4.8 2.36 0.69 5 Discussion The best result with the inverter was achieved at an inverter frequency of 45 Hz. The test results demonstrate that there may exist an optimum duty cycle, which is not 100 percent, when an inverter is used. In addition to using the inverter, the supply voltage was optimized and found to be 90V. 34 ------- Prototype Test Results May 1994 III.A.3. Voltage Regulator i III.A.3.O. Green Plug—New Top-Freezer Refrigerator The "Green Plug" is a commercially available voltage regulator. ' t Baselinfe Unit The baseline unit was a 20 ft3 top-freezer automatic-defrost R/F ! manufactured by Whirlpool in 1992, model number ET20ZKXZW. Prototype Unit Baseline R/F was connected to a 115V and 120V power supply via the ! Green Plug. t . ; Table III.3 Green Plug—New Top-Freezer Refrigerator i Green ; Baseline Plug Input Voltage (V) Energy Consumption (kWh/24h) FF/FZ Temperature (°F) Duty Cycle % Energy Reduction 115 2.47 37.1/4.0 0.54 115 2.37 35.2/4.9 0.54 4 ; . • '• . - ' - - * i - ; V " i Green i Baseline Plug i . o Input Voltage (V) Energy Consumption (kWh/24h) FF/FZ Temperature (°F) Duty Cycle % Energy Reduction 120 2.41 38.2/8.4 0.48 120 , 2.40 38.7/8.6 0.45 0 Discussion Generally, test results with this refrigerator showed performance i changes of about 2+3 percent when the Green Plug was used. Similar results have been found by Consumers Union. [10] 35 ------- Energy-Efficient Refrigerators IILA.3.b Green Plug—Side-by-Side Refrigerator The Green Plug is a commercially available voltage regulator. Baseline Unit The baseline unit was a 1975 Sears 19 ft3 side-by-side R/F, model number 106-7650511. Prototype Unit The baseline unit was connected to a 115V and 120V power supply via the Green Plug. Table ILIA Green Plug—Side-by-Side Refrigerator ... ' v i : •! * .'(•••-.••. '.' : ' : ,| • I i Green ; : ' ; ; 1 Baseline r Plug Input Voltage (V) Energy Consumption (kWh/24h) FF/FZ Temperature (°F) Duty Cycle % Energy Reduction 120 5.34 34.1/8.2 0.67 120 5.35 34.4/8.4 0.69 0 ! -.{ '. ! ! - l : : - | ; ' Green; j -j 'j ' Baseline Plug Input Voltage (V) Energy Consumption (kWh/24h) FF/FZ Temperature (°F) Duty Cycle % Energy Reduction 120 6.11 30.1/3.8 0.75 120 5.75 30.9/4.2 0.68 6 Discussion Generally, test results with this refrigerator showed performance changes of about minus two to six percent when the Green Plug was used. Only at 120V and under severe operating conditions (high temperature lift) were savings of 6 percent found. These results are also consistent with results found by Consumers Union. [10] 36 ------- .Prototype Test Results May 1994 III.A.4 Hot Water Refrigerator Baseline Unit The baseline R/F was an 18 ft3 top-freezer automatic-defrost unit produced by Whirlpool, model number ET18ZKXZWOO. Prototype Unit A water-cooled condenser was added before and in series with the condenser of the baseline R/F. The water loop for the water-cooled i condenser was equipped with a 5-gallon water tank and a circulation I pump. Whenever the refrigerator was in operation, the pump operated ! and the condenser fan was turned off. If the water temperature in the I tank rose above the set point, the pump would turn off, and the t condenser fan would come on. The water-cooled condenser was a tube- j in-tube, counter-flow heat exchanger with refrigerant in the inside tube. j Outside and inside tubes were 0.375" and 0.125" in diameter, and the I condenser was about 120" long. Table III.5 Hot Water Refrigerator i Baseline Prototype Energy Consumption (kWh/24h) FF/FZ Temperature (°F) Water Flow Rate (g/s) Initial Temperature in Water Tank (°F) Final Temperature in Water Tank (°F) Heat Recovered to Water Tank (kWh/24h) Duty Cycle 1.86 38.9/3.5 n/a n/a n/a n/a 0.46 2.09 36.0/4.1 14.5 : 72 118 1.26 0.33 Discussion While the energy consumption of the prototype R/F was higher than for ; the baseline, the heat recovered by the water-cooled condenser reduced j the energy requirement of the water heater. Results of a simulation of a domestic water heater combined with the measured refrigerator performance show net energy savings of 10 to 15 percent for the ! combined system. 37 ------- Energy-Efficient Refrigerators III.B. IMPROVED REFRIGERANTS III.B.1 Improved Refrigerants—Hydrocarbon Blends Baseline Unit The baseline unit was a 20 ft3 top-freezer automatic-defrost R/F produced by Whirlpool, model number ET20ZKXZW. Prototype Unit A mixture of n-butane (R-600) and propane (R-290) was used as a refrigerant in the original refrigerator. The capillary tube length and charge were optimized. A sight glass at the condenser outlet and two pressure transducers were also added. The additional capillary tube had a diameter of 0.026". Table III.6 Hydrocarbon Blends Baseline R-600 and R-290 1 ' i i . " i - -i Charge (g) Extra Cap. Tube (ft) Energy Consumption (kWh/24h) FF/FZ Temperature (F) Duty Cycle % Energy Reduction 240 0 2.47 37.1/4.0 0.54 80 (30/70) 5 2.30 39.4/3.3 0.33 7 Discussion There are a number of advantages that result from hydrocarbon use: energy savings up to seven percent compared to R-12 as the refrigerant, charge reduction to a third of that of R-12, and a lower pressure ratio than that of R-12. The energy savings can be improved by taking advantage of the temperature glide (which was not done here). The charge can also be reduced further with better designs, thereby reducing the flammability risk. It should be noted that the mixture concentration may vary considerably due to preferential oil solubility and storage effects in components. [11] 38 ------- Prototype Test Results May 1994 III.B.2 Improved Refrigerants—Cyclopropane Baseline Unit The baseline R/F was an 18.0 ft3 top-freezer automatic-defrost unit i manufactured by Whirlpool. Prototype Unit Only the refrigerant, amount of charge, and the length of the capillary i tube were changed. j Table IIL7 Cyclopropane Baseline Cyclopropane Charge (g) Energy Consumption (kWh/24h) FF/FZ Temperature (°F) Duty Cycle % Energy Reduction 156 2.20 38.5/4.4 0.52 100 2.05 38.9/4.4 0.47 7 Discussion Cyclopropane showed a seven percent decrease iri energy consumption compared to the baseline with R-12. The volummetric capacity of cyclopropane is 17 percent higher than that of R-12. Since the j compressor remained unchanged, the higher volummetric capacity i resulted in a reduction of the compressor run time. The discharge pressure of cyclopropane increased by 10 percent, while the suction , pressure was similar to that of R-12. [12] ! ERA predicted a four percent energy reduction when HFC-134a was replaced by cyclopropane. [2] 39 ------- Energy-Efficient Refrigerators III.B.3 Improved Refrigerants—HFC-134a and HFC-152a Original Unit The original unit was an 18.0 ft3 top-mounted automatic-defrost R/F built by GE, model number TBX18P. Prototype Unit The original compressor was replaced with a RG108-1 compressor for HFC-134a tests. It was then replaced with a TG108-1 compressor for HFC-152a tests. Both compressors came from AMERICOLD. • Table HL8 Minimum Energy Consumption of the Optimized Systems System bfype . '. \ HFC-134a HFC-152a Min. energy consumption (kWh/day) Avg. instantaneous power (on time) (W) Compressor on-time (min) Total cycle time (min) Additional capillary tube length (ft) Refrigerant charge (g) Avg. freezer comp. temperature (°F) Avg. food comp. temperature (°F) Avg. evap. pressure during on time (psia) Avg. cond. pressure during on time (psia) 1.83 172.4 23.0 52.0 7.0 200 5.6 40.8 15.1 174.0 1.79 174.0 21.0 49.0 18.0 120. 5.1 40.3 13.3 163.3 Table III.9 Calorimeter Data for the Two Compressors ' ;- .:•!;. I . . ' ! '• : :. Refrigerant i HFC-134a HFC-152a ' : ' [ ! i Compressor model # Oil type Evaporation teinperature (°F) Evaporation pressure (psia) Condensing temperature (°F) Condensing pressure (psia) Capacity (BTU/h) EER RG108-1 RL212B (Ester) -10.4 16.5 129.9 213.4 759.9 4.78 TG108-1 100DL (alkylbenzene) -9.4 15.4 129.8 190.3 824.7 4.93 Discussion The HFC-152a R/F test has two percent lower energy consumption than the HFC-134a R/F test. The calorimeter tests show a three percent lower EER and an eight percent lower capacity for the HFC-134a compressor. The lower capacity of the compressor is reflected in the longer run time for the HFC-134a R/F. When the lower EER of the HFC-134a compressor is considered, both systems have the same performance. [13] 40 ------- Prototype Test Results Mai/1994 III.B.4 Improved Refrigerants—HCFC-22 and HFC-152a Blends Baseline Unit The baseline R/F was a GE 18 ft3 top-freezer automatic-defrost unit. i Prototype Unit There were essentially no changes made to the refrigerator, except i changes to the capillary and the addition of measurement probes (two pressure transducers and one sight-glass). Table 111.10 HCFC-22 and HFC-152a Blends ' 1 ' : i Babeline 13% HCFC-22 and 87% HFC-152a Charge (g) Energy Consumption (kWh/24h) FF/FZ Temperature (°F) 1 I Duty Cycle % Energy Reduction 350 2.11 44.3/5.0 0.48 207 (27&180) 2.03 43.7/4.8 0.48 4 Discussion Several mixture compositions were tried to find the mixture of 13 percent HCFC-22 and 87 percent HFC-152a. This best mixture led to an optimum energy savings of four percent. [12] 41 ------- Energy-Efficient Refrigerators m.C. IMPROVED CYCLE IH.C.l Lorenz-Meutzner Cycle IILC.l.a Lorenz-Meutzner Cycle—Zeotropic Refrigerant Mixtures Baseline Unit The baseline R/F was a 20.0 ft3 side-by-side unit produced by Whirlpool. Prototype Unit The original evaporator was replaced by a counter-cross-flow evaporator, and a natural convection evaporator was added to the fresh food compartment. The total internal volume of the two evaporators was 72 percent of the original evaporator volume, resulting in a reduction of the charge. The original 10W freezer evaporator fan was replaced with a 7W unit, and a small 1W DC fan was placed in the fresh food cabinet to eliminate temperature gradients. A combination of two counter-current tube-to-tube heat exchangers (high and low temperature) and an adiabatic capillary tube replaced the conventional suction line heat exchanger. The original reciprocating compressor and condenser were used. The original compressor oil, a 150 SSU mineral oil (naphthenic), was used for tests involving R-12. A synthetic oil (alkylbenzene) was used with the zeotropic refrigerant mixture. A commercial filter dryer was installed in the liquid line after the condenser. Additional details on the various components can be found in reference [14]. Table III.ll Lorenz-Meutzner Cycle—Zeotropic Refrigerant Mixtures Baseline ' (R-12) :. 65% HCFC-22 •- and 35%HCFC-123 71% HqFC-22 and 29% HCFC-141b 60% HCFC-22 and 40% HCI-C-123 Energy Consumption (kWh/24h) FF/FZ Temperature (°F) Duty Cycle % Energy Reduction 2.44 36.6/4.5 0.57 2.17 36.2/5.0 0.53 11 2.20 40.0/4.9 0.51 10 2.26 38.0/4.9 0.58 7 Discussion This prototype demonstrates that the Lorenz-Meutzner cycle works well in a side-by-side refrigerator/freezer. The natural-convection food-compartment evaporator caused significant temperature stratification that could be eliminated with a 1W fan. Consequently, a forced-convection evaporator is recommended for the food compartment in a side-by-side unit. 42 ------- Prototype Test Results May 1994 IILC.l.b Lorenz-Meutzner Cycle—Hydrocarbon Blends Baseline Unit The baseline unit was an 18.0 ft3 top-freezer automatic-defrost R/F built : by Whirlpool, model number WT18NKYO. Prototype Unit A natural convection food compartment evaporator, a counter-flow | freezer evaporator, and a suction line heat exchanger were added to the 1 baseline R/F. 1 Table IIL12 Lorenz-Meutzner Cycle—Hydrocarbon Blends Baseline Baseline Cycle Baseline LM 1 ,LM 2 L-M L-M L-M L-M ! i ; ' Refrigerant Charge (g) Energy Consumption (kWh/24h) f FF/FZ T emperature % F^nergy Reduction Test Date R-12 300 1.83 38.1 / 4.7 10/91 original R-12 310 1.69 38.5/ 5.0 8 * 09/92 R-12 360 1.84 38.1/ 4.7 -1 * 05/93 R-290/ C5H12 180 (50/50) 1.54 40.4/ 4.8 16 R-290/ HCFC-123 180 (50/50) 1 1.52 38.9/ 4.7 17 : R-290/ R-600 145 (48/52) 1.52 38.8/ 5.1 17 R-290/ R-600/ 157 (42/S9/ 19) 1.50 40.2/5.1 18 * After conversion to Lorenz-Meutzner cycle Discussion Hydrocarbon mixtures in the Lorenz cycle save energy in the range from I 16 to 18 percent as compared to R-12 in a top-freezer automatic-defrost I refrigerator. If it is considered that the refrigerator insulation tends to ! age over time (increasing of thermal conductivity), which may be t indicated by the difference in the baseline tests LM1 and LM2 with j otherwise identical hardware, then the savings will reach 23 to 25 I percent. 43 ------- Energy-Efficient Refrigerators ERA predicted 18 percent energy reductions for similar R/Fs with natural convection evaporators in the fresh food compartment. This is in agreement with the test results. 44 ------- Prototype Test Results May 1994 III.C.l.c Lorenz-Meutzner Cycle Baseline Unit The baseline R/F was a 19.8 ft3 top-freezer automatic-defrost unit I produced by Whirlpool, model number ET20ZKXZW. i Prototype Unit A counter-cross-flow condenser (forced convection), counter-flow freezer | evaporator (forced convection), counter-flow food compartment I evaporator (natural convection) were added. An inter-cooler between 1 the freezer and fresh food evaporators was not used. 1 Table IIL13 Lorenz-Meutzner Cycle I 1 Heater On Off Off Off On On Refrigerant FF/FZ Temperature (PF) Energy Consumption (kWh/24h) % Energy Reduction** R-12 41.9/5 2.17 R-12 38.6/5 2.05 Mixture 1* 38.5/4.5 1.74 15 Mixture 2* 42.0/5.2 1.66 19 R-12 41.8/4.8 !- 2.28 Mixture 2* 42.3/4.8 1.92 16 Mixture 1 is HFC-134a (56%)/HCFC-123 (31%)/R-290 (4%)/HFC-32 (9%), and (Mixture) 2 is R-290 (65 %)/HCFC-123 (35%). • • - ; i | Compared •with the test result using R-12. Discussion The R-12 test was repeated (second to last column) to account for the ! aging of the cabinet and any other deterioration of the insulation that may have occurred during the numerous modifications. The energy 1 savings are calculated based on the respective baseline test (either with I the heater on or off). The savings of the last test are based on the latest : baseline. Test results show that at least 15 percent energy savings can i be achieved with this version of the Lorenz-Meutzner cycle. 45 ------- Energy-Efficient Refrigerators III.C.2 Modified Lorenz-Meutzner Cycle III.C.2.a Modified Lorenz-Meutzner Cycle—U.S. Refrigerator The modified Lorenz-Meutzner cycle has three-way internal heat exchangers in the food and freezer compartments, where heat is mutually exchanged between the compartment air, refrigerant condensate, and evaporating refrigerant. In the original Lorenz-Meutzner Cycle, heat is internally exchanged between the compartment air and refrigerant vapor, while the refrigerant condensate line is bypassed. Baseline Unit The baseline R/F was a 19.8 ft3 top-freezer automatic-defrost Whirlpool (Kitchen Aid) unit, model number KTRS20KXWH10. Prototype Unit A modified Lorenz-Meutzner cycle with internal heat exchange in the evaporators, counter-cross-flow condenser and freezer evaporator, natural-convection food evaporator, and intercooler added. The refrigerator/freezer was equipped with the original rotary compressor and energy-saving valve. Table IIL14 Modified Lorenz-Meutzner Cycle—IT.S. Refrigerator ''.'•: : ;; Baseline - i Prototype Refrigerant Energy Consumption (kWh/24h) FF/FZ Temperature (°F) % Energy Reduction R-12 1.86 38.1/5.1 R-290/HCFC-123 1.55 38.6/4.1 17 Discussion The results indicate that the daily energy consumption decreased by up to 17 percent without considering the defrost cycle. Many other CFC-free refrigerant mixtures were also tested with significant energy savings, in the same 17 percent savings range. 46 ------- Prototype Test Results May 1994 III.C.2.b Modified Lorenz-Meutzner Cycle—Chinese Refrigerator Baseline Unit The baseline R/F was a top-freezer 6.4 ft3 automatic-defrost model produced by the ShangLing Refrigerator Co., model number BCD-180. Prototype Unit Modification similar to those described in Section IH.C.2.a were made. The evaporator was constructed of 5/16 inch O.D. aluminum/copper ! tubing in a cross-counter-flow pattern with 40-45 plate fins. The ! resulting heat exchanger was 9 inches deep in the direction of air flow I with 12.5 inch x 2 inch cross-sectional area. f : Table 111.15 Modified Lorenz-Meutzner Cycle—Chinese Refrigerator Refrigerant Baseline R-12 Prototype R-290/ HCFC-123 Energy Consumption (kWh/24h) 1.29 1.16 FF/FZ Temperature (°F) 38.7/5.0 38.1/5.0 ' % Energy Reduction 10 Discussion The results indicate that the daily energy consumption decreased by up , to 10 percent. Since this Chinese refrigerator had much smaller internal j volume, there was not much room for optimizing the evaporators. Also, I the condenser was located in the foam insulation and was not a counter- flow design. Considering these limitations, the energy savings were quite good, although not as high as found in the American R/F. [15] 47 ------- Energy-Efficient Refrigerators III.C.3 Dual-Loop System Baseline Unit Prototype Unit The baseline R/F was a 19.8 ft3 top-freezer automatic-defrost unit manufactured by Whirlpool. A dual-loop system with two separate vapor compression cycles, one for the freezer and one for the food compartment, were added. The freezer compartment cycle included a 4.0 EER reciprocating compressor, which was placed at the left outside of the cabinet, the original evaporator and fan, mounted in the original position, and a natural convection condenser located on the back of tine cabinet. The food compartment cycle consisted of a 3.65 EER reciprocating compressor, located in the original compressor compartment, a new counter-flow heat exchanger with a 6 W fan, and a new natural convection condenser. To reduce heat transfer between the two compartments, the top side of the food and the bottom side of the freezer compartments were insulated with a 1-inch thick glass wool mat. The compressor oil was changed from a mineral oil with 3GS viscosity to a 1GS mineral oil to compensate for the lower operating temperatures. Additional details can be found in reference [16]. Table 111.16 Dual Loop System I ! Baseline ' DuallLoop Energy Consumption (kWh/24h) FF/FZ Temperature (°F) Duty Cycle % Energy Reduction 1.98 40.5/3.7 0.47 1.87 (1.3.0 in FF + 0.57 in FZ) 39.6/3.7 0.51 for FZ/0.22 for FF 4 Discussion The best result achieved with the dual loop system showed a four percent improvement of the total energy consumption over the baseline. The compressors used in both cycles were smaller and lower EER than the original rotary compressor (EER = 4.9). Energy savings of more than 20 percent could be possible, if compressors with the same EER as the original compressor were available. The reported savings exclude defrost. Higher energy savings can be expected when defrost is included. This effort continued for an additional 12 months with the 48 ------- Prototype Test Results May 1994 best result being a 4 percent reduction in energy consumption. Accounting for foam aging, the result would have been higher. ERA calculations for the dual loop have predicted a two percent energy reduction. The savings were smaller because forced convection evaporators and condensers were used. [2] 49 ------- Energy-Efficient Refrigerators III.C.4 Two-Stage Refrigerator Baseline Unit The baseline model was built at U. Md. It consisted of an approximately 20 ft3 top-freezer refrigerator that was housed in an insulated wooden box. Prototype Unit A forced convection food compartment evaporator, forced convection freezer evaporator, and condenser were used. Two compressors were used in series. The first pumped refrigerant from the freezer evaporator to the food compartment evaporator pressure level, the second from the fresh food pressure level to the condenser pressure level. Table 111.17 Two-Stage System •i^MMl Energy Consumption (kWh/24h) FF/FZ Temperature (°F) Duty Cycle FF/FZ Compressor EER Charge (g) % Energy Reduction r - " Baseline j pfwo-Stage 3.30 43.9/5.2 0.72 4.4 480 3.20 38.3/5.3 0.62 4.2/3.4 316 3 Discussion The test results show a three percent energy savings over the single stage configuration. Considering that the food compartment temperature was considerably lower than in the baseline test, another three percent could have been gained. Finally, accounting for the lower compressor EER would result in a total energy savings of about 20 percent. 50 ------- Prototype Test Results May 1994 III.C.5 Kopko Cycle The Kopko cycle represents a method of achieving energy savings with two evaporators in 3 single circuit without the use of mixtures or special control valves. The basic set-up uses a freezer evaporator and fresh-food evaporator connected in series, each with its own fan. The controls run one evaporator fan at a time. Only the freezer fan operates when cooling the freezer; and only the fresh-food compartment fan operates when cooling the fresh-food compartment. The evaporators are installed to minimize natural convection of air when the fans are off. The normal sequence is to cool the fresh-food compartment first, then the freezer. This set-up uses the higher evaporator pressures that normally occur at the beginning of the compressor on time to cool the fresh-food compartment. Baseline Unit The baseline unit was an 18 ft3 top-freezer automatic-defrost R/F manufactured by Whirlpool, model number ET18NKXYW. Prototype Unit A forced convection food compartment evaporator was added to the • system. Capillary tube length was optimized and measurement probes j were added. The control logic was changed. Lastly, the compressor I was exchanged as indicated in the table below. [17] ; Table 111.18 Kopko Cycle Baseline Kopko i Energy Consumption (kWh/24h) FF/FZ Temperature (°F) Duty Cycle Compressor HER Charge (g) % Energy Reduction 1.78 38.4/4.9 0.45 FGV80AW(SINGLE) 4.91 177 1.24 39.0/5.1 0.43 AMERICOLD HG107 5.52 360 30 Discussion The use of the Kopko configuration leads to considerable energy i savings. When the higher compressor EER is excluded, the new configuration produces an 18 percent increase in performance. , The following six tables describe all of the intermediate modifications to i the Kopko system and the respective test results. 51 ------- Energy-Efficient Refrigerators Table IIL19 Kopko Cycle—First Modification ' Baseline First Modification '-. > 1 i i i . 1 Size Compressor Freezer Evaporator Type Total Area Flow Fan Food Evaporator Type Total Area Flow Fan Condenser Capillary Tube SLHX Fan Control R-12 Flow Path Direction R-12 Charge (g) Two-Way Switch Model # Power On-time Delay Relay Model # Power Filter Dryer Sight-glass 18ft3 FGV80AW Forced Convection Plate Fin and Tube 2,500 in2 Cross-Flow 40 - 50 cfm, 8 - 12 W N/A Natural Convection ~8' (0.026" ID) 6'8" 0.026" ID by 0.313" OD N/A N/A 177 N/A N/A Original N/A Same as Baseline Same as Baseline Forced Convection Spiny Fin and Tube 1,457 in2(0.94 m2) Counter-Flow Same as Baseline Forced Convection Plate Fin and Tube 2,500m2 Cross-Flow 65cfm, 7W Pewee Boxer Model* 4715PS-12T-B10 Same as Baseline 9'6" (0.026" ID) in FZ 10' (4' located in FF) 0.125" by 0.313"OD FZ Fan First with Timer , FZ to FF Evaporator 230 Potter-Brumfield KUP-5A15-120 2W Dayton Elect. MFG. Co. 6X601F (Range 9-900sec) 3 W ALCO EK - 032 Installed 52 ------- Prototype Test Results May 1994 Table 111.20 Kopko Cycle—First Modification Test Results Energy Consumption ,(kWh/24h) Baseline 1.78 First Modification 1.67 ^Z/FF Temperature (°F) 4.9/38.4 4.7/38.2 kTD Controller Set Point, FZ/FF (°F) jHysterisis, FZ/FF 5.5/- 1.4/- 4.5/38.55 0.4/0.3 Puty Cycle 0.45 0.42 % Energy Reduction 53 ------- Energy-Efficient Refrigerators Table 111.21 Kopko Cycle—Second Modification First Modification Second Modification : Compressor Freezer Evaporator Type Total Area Flow Fan Food Evaporator Type Total Area Flow Fan Condenser Capillary Tube SLHX Fan Control R12 Flow Path Direction R12 Charge (g) Two-Way Switch On-time Delay Relay Filter Dryer Sight-glass Special Insulation Mullion FZ Evaporator Cover FGV80AW Forced Convection Spiny Fin and Tube 1,457 in2 Counter-Flow 40 - 50 cfm, 8 - 12 W Forced Convection Plate Fin and Tube 2,500 in2 Cross-Flow 65 cfm, 7 W Pewee Boxer Model* 4715PS-12T-B10 Natural Convection 9'6" (0.026" ID) in FZ 10' (4' located in FF) 0.125" by 0.313"OD FZ Fan First with Timer FZ to FF Evaporator 230 Installed Installed Installed Installed N/A FGV80AW .' Forced Convection Spiny Fin and Tube 2,853 in2 (1.84 m2) Counter-Flow 26 cfm, 4 W Forced Convection Plate Fin and Tube 3,661 in2 (2.36 m2) Cross-Flow 65 cfm, 7 W Pewee Boxer Model* 4715PS-12T-B10 Natural Convection 8'0" (0.026" ID) in FZ 6'8" 0.026'TD by 0.313"OD FF Fan First FZ to FF Evaporator 300 Installed N/A Installed Installed 1" Foam Glass Wool 54 ------- Prototype Test Results "May~1994 Table 111.22 Kopko Cycle—Second Modification Test Results : " =: 1- Eirst Second ; i , Modification . Modification Energy Consumption (kWh/d) FZ/FF Temperature (°F) RTD Controller Set Point, FZ/FF (°F) Hysterisis, FZ/FF ; Pressure (psia) High Side- Low Side Temperature (°F) Condenser FZ Evaporator FF Evaporator On/Off-Time (min) FF On-Time (min) Duty Cycle % Energy Reduction from Baseline 1.67 4.7/38.2 4.5/38.55 0.4/0.3 . 161.6 15.5 105.2 -21.3 9.5 12.8/18.0 - (Fan on once) 0.42 6 1.56 5.0/38.3 5.9/36.9 1.0/0.2 158.1 16.2 113.0 -15.8 -3.9 13.5/19.7 4.5 (Fan on twice) 0.41 1 12 55 ------- Energy-Efficient Refrigerators Table 111.23 Kopko Cycle—Third Modification and Test Results : • - : • ' 1 . .' ' 1 • ' ' • • Second Modification Third Modification Energy Consumption (kWh/d) FZ/FF Temperature RTD Controller Set Point, FZ/FF (°F) Hysterisis, FZ/FF Pressure (psia) HigltySide Low Side Temperature (°F) Condenser FZ Evaporator FF Evaporator Compressor Model* Capacity EER Oil R12 Charge (g) On/Off-Time (min) FF On-Time (min) Duty Ctcle % Energy Reduction from Baseline 1.56 5.0/38.3 5.9/36.9 1.0/0.2 158.1 16.2 113.0 -15.8 -3.9 Reciprocating FGV80AW (EMBRACO) 820 4.91 Mineral, 3GS 300 13.5/19.7 4.5 0.41 12 1.29 5.1/ 39.2 . 5.35/36.25 0.7/0.7 152.2 15.5 97.5 -17.5 12.3 Reciprocating HG-107 (AMERICOLD) 700 5.5 Mineral, 1GS 320 13.3/16.3 5.5 , 45 28 56 ------- Prototype Test Results May1994 Table 111.24 Kopko Cycle—Fourth Modification and Test Results I 1 Third Modification Fourth Modification ; - Energy Consumption (kWh/24h) FZ/FF Temperature ! (°F) ! RTD Controller | Set Point, FZ/FD (°F) ! Hysterisis, FZ/FD Pressure (psia) High /Low Side Temperature (°F) Condenser FZ/FF Evaporator Compressor 1 Model* [ Capacity EER Oil : R12 Charge (g) Filter Dryer Sight-glass On/Off-Time (min) FF On-Time (min) Duty Cycle % Energy Reduction from Baseline 1.29 5.1/39.2 5.35/36.25 0.7/0.7 152.2/15.5 97.5 -17.5/12.3 Reciprocating HG-107 (AMERICOLD) 700 5.5 Mineral, 1GS 320 Installed Installed 13.3/16.3 5.5 0.45 28 1.24 5.1/39.0 4.0/35.2 1.5/0.6 150.1/16.2 95.0 -15.2/42.8 Reciprocating HG-107 (AMERICOLD) 700 5.5 Mineral, 1GS 320 Removed Removed 20.8/28.0 7 0.43 30 57 ------- Energy-Efficient Refrigerators 58 ------- Prototype Test Results May 1994 IV. SYSTEM AND CABINET MODIFICATIONS Several super-efficient prototype units have been built and tested combining modifications to both the system and cabinet. These units are described in this section. 59 ------- Energy-Efficient Refrigerators IV.A DOUBLE INSULATION AND LORENZ-MEUTZNER CYCLE Baseline Unit The baseline model was a 20 ft3 top-freezer automatic-defrost R/F produced by Whirlpool. This was the same unit described in Section II.A.1. Prototype Unit A series of modifications were made to the prototype unit. These included adding double insulation (see II.A.1), adding a high-efficiency compressor, adding a modified Lorenz-Meutzner cycle with a HCFC-123 and R-290 refrigerant blend, and reducing the gasket region heat leak. The results of each step in the path follow. Details of individual steps are then presented. [18] Table W.l Double-Insulated, Lorenz-Cycle Refrigerator In$ulatlon Standard Double Double Double Double DOUBLE Compressor* Cycle Door Seal Refrigerant Charge (g) FF/FZ Temp. (°F) Duty Cycle Energy Consump. (kWh/24h) Energy Consump. including defrost % Energy Reduction Total % Energy Reduction Standard Standard Standard R-12 38/5 1.86 Standard Standard Standard R-12 220 37.0/5.3 0.36 1.36 1.47 27 27 High Eff. Standard Standard R-12 220 37.2/5.4 0.39 1.26 1.38 7 32 High Eff. Lorenz Standard R-12 410 36.4/5.9 0.39 1.25 N/A 1 33 High Eff. Lorenz Standard HCFC-123 and R-290 210 38.6/5.4 0.26 1.05 1.20 16 44 High Eff. Lorenz Improved HCFC-123 and R-290 210 38.5/5.5 0.25 1.01 1.14 4 46 *Sce Table IV.2. for additional information. Discussion The next four sections provide design details Detailed comparison of the test results and a improved door seal are also attached. of the prototypes tested. drawing showing the 60 ------- Prototype Test Results May 1994 IV.A.1 Double Insulation These modifications are described in Section II.A.I. IV.A.2 High-Efficiency Compressor The calorimeter test data for the high-efficiency compressor were provided by the manufacturer. Table IV.2 compares the original rotary compressor with the high efficiency reciprocating compressor. The EER of the new compressor was about 12 percent higher than that of the conventional compressor used in the original thick wall unit. [18] , Table IV.2 High-Efficiency Compressor ' \ Original High Efficiency Compressor Compressor Model Type Oil Oil Viscosity EER (BTU/W-h) Capacity (BTU/h) Power (W) RA53L11RA Rotary Alkylbenzene 3GS 4.80-4.86 850-867 177 HG107 Reciprocating Mineral Oil 1GS 5.50-5.54 , 703.2-713.4 129 61 ------- Energy-Efficient Refrigerators IV.A.3 Modified Lorenz-Meutzner Cycle A modified Lorenz-Meutzner cycle was incorporated into the R/F. See section III.C.l.c for additional details. Table IV.3 compares the specifications of the standard and new cycles. Table IV.3 ModifiedTLorenz-Meutzner Cycle Double Insulated with High Efficiency Compressor Modified Lorenz-Meutzner Cycle Size Compressor Compressor Oil Freezer evaporator Cabinet evaporator Condenser Suction line HX Low temp. HX 19.9 cubic feet HG107 Alkylbenzene Forced convection tube and fin, 18 tube passes, 26" each pass, 3/8" OD, 77 fins, cross-flow type None Forced convection 0.026" ID capillary tube soldered to 5/16" OD suction line None Less than 19.9 cubic feet (considering space of cabinet evaporator) HG107 Mineral oil Forced convection tube and fin, 18 tube passes, 25". each pass, 3/8" OD counter-cross flow Natural convection copper flat- plate, 28" by 26", copper plate two side with thickness 1/32", total surface area 1456 in2 Forced convection, modified to counter flow 1/8" OD soldered to 5/16" OD suction tube, same length as the original length 25" long 3/8" OD and 1/8" OD tube soldered together, two passes 62 ------- ; , Prototype Test Results : May 1994 IV.A.4 Improved Gasket t The cabinet flange was modified to reduce heat leakage into the cab:inet as described in Section II.C.l. A drawing of the modified gasket region follows. Figure IV.l Schematic Representation of Improved Gasket insulation tape 2 inches in width 1/8 inch in thickness Freezer Compartment Fresh Food Compartment Front View 63 ------- Energy-Efficient Refrigerators IV.B DOUBLE INSULATION AND KOPKO CYCLE Baseline Unit The baseline model was the 20 ft3 R/F described in Section II.A.1. Prototype Unit Double insulation (section II.A.I) and the Kopko cycle (Sectidn III.C.5) were added to the baseline model. Table IV.4 Double-Insulated, Kopko-Cycle Refrigerator \ : : ; Baseline Double Insulation ; Kopko Energy Consumption (kWh/24h) FF/FZ Temperature (°F) Duty Cycle Compressor EER % Energy Savings Total % Energy Savings 1.86 38.1/5.1 0.45 RA53L11RA(SINGLE) 4.9 1.43 38.7/5.2 0.34 RA53L11RA(SINGLE) 4.9 23 ... 23 1.29 38.2/5.0 0.34 FN45R80T 4.5 10 31 Discussion Accounting for the change in the compressor EER, the total energy savings based on the Kopko concept amounts to 19 percent. This would result in nearly a 40 percent reduction for the total modification. The following four tables describe all of the intermediate modifications to the system and the respective test results. 64 ------- Prototype Test Results May 1994 Table IV.5 Specifications for the First Modification Baseline First Modification Size Wall Insulation Compressor Model* Capacity EER Oil Freezer Evaporator Type Total Area Flow Fan Food Evaporator Type Total Area Flow Fan Condenser ; Capillary Tube SLHX Fan Control I R-12 Flow Path ; Direction R-12 Charge Two- Way Switch Model # Power Filter Dryer Sight-glass 20ft3 Thick wall Rotary RA53L11RA 870.7 BTU/h(255.2 W) 4.91 Mineral, 4GS Forced convection Plate fin and tube 3,661in2 Cross-flow 40 - 50 cfm, 6 - 10 W N/A Forced convection ~ 8 ' (0.026" ID) 0.026" ID by 0.313" OD N/A N/A 205.5 g N/A Original N/A Same as baseline Same as baseline Rotary RA48L83TE 787 Btu/h(230.7 W) 5.01 Mineral, 4GS Forced convection Plate fill and tube 4,265 in2(3.96 m2) Counter-flow 65 cfm, 7W Forced convection Plate fin and tube 4,168 in2(3.87 m2) Counter-flow 65 cfm, 7 W Same as baseline 7'0" (0.026" ID) in FZ 0.125" by 0.313"OD FF fan first FZ to FF evaporator 410 g Potter-Brumfield KUP-5A15-120 2 W Same as baseline N/A 65 ------- Energy-Efficient Refrigerators Table JV.6 Test Result for the First Modification : 1 - - j 1 • i . , : ! • i j Double Insulation j: First Modification Energy Consumption (kWh/d) FZ/FF Temperature (°F) Total Savings (%) Net Saving On/Off Time (min) FF On-Time (min) On-Time Ratio (%) RTD Controller Set Point, FZ/FF (°F) Hysterisis, FZ/FF 1.43 5.2/38.7 - 18.1/35.5 - 33.8 5.857 - 1.27- 1.24 5.2/38.2 12.8 10.8 17.0/32.0 5.6 34.7 4.5/39.0 1.5/0.2 Table IV.7 Compressor Comparison for Kopko Modifications : ! : ! : 1 ' •; ! ; First ; , Second Baseline Modification Modification Compressor Model # Capacity (BTU/h) EER (%) Oil Rotary Matsushita RA53L11RA 870.7(255.2 W) 4.91 Mineral, 4GS Rotary Matsushita RA48L83TE 787.0(230.7 W) 5.01 (+ 2.0) Mineral, 4GS Rotary Matsushita FN45R80T 715.0(209.5 W) 4.5 (- 8.4) Mineral, 4GS 66 ------- _"-"••' Prototype Test Resutis Way'1994 IV.C DOUBLE INSULATION AND ALTERNATE REFRIGERANTS IV.C.1 HFC-152a Baseline Unit The baseline model was an 8.5 ft3 bottom-freezer R/F produced by i Qingdao Haier in China, model number BCD-220. The standard cycle , includes two evaporators and a single compressor with a switching j valve to control refrigerant flow. I Prototype Unit Double insulation and cycle modifications were made to the unit. I Added insulation was 0.8 inches on the sides, back, and bottom and 0.6 ; inches to the doors. Cycle improvements included, adding a counter- { flow condenser (natural convection), a counter-flow freezer evaporator j (three-way heat exchanger, natural convection), and a food compartment j evaporator (natural convection). An inter-cooler was not added between s the freezer and food compartment evaporators. A high-efficiency | compressor obtained from AMERICOLD (TG105-12) was also used. ; Table IV.8 Increased Insulation with Refrigerants HFC-152a Refrigerant R-12 HFC-152a Energy Consumption (kWh/24h) Compressor EER FF/FZ Temperature (°F) % Energy Reduction 1.70 3.62 38.0/5.0 0.96 4.48 38.0/5.1 44 Discussion The results show that the combination of modifications reduced the energy consumption by about 44 percent. 67 ------- Energy-Efficient,Refrigerators IV.C.2 Hydrocarbon Mixtures Baseline Unit The baseline unit was the same as described in the previous section. Prototype Unit The modifications were the same as above except hydrocarbon refrigerants were used. Table IV.9 Increased Insulation with Hydrocarbon Refrigerants Refrigerant Energy Consumption (kWh/24h) R-290 (68i%) and R-2^0 (63%) and R-600 (32%) R-600 (37%) 1.70 0.80 0.83 FF/FZ Temperature (°F) 38.0/5.0 37.5/4.8 38.1/5.0 % Energy Reduction 53 51 Discussion Test results show that an additional 10 percent energy savings can be achieved using hydrocarbon mixtures as compared to the system using HFC-152a. 68 ------- Prototype Test Results May 1994 V. REFERENCES 1. EPA Refrigerator Analysis Program (ERA): User's Manual, Report Number EPA-430-R-93- 007, U.S. Environmental Protection Agency, June 1993. 2. Multiple Pathways to Super-Efficient Refrigerators, Report Number EPA-430-R-93-008, U.JS. Environmental Protection Agency, June 1993. i 3. Carbon Black in Appliance Foam Insulation, }. S. Pisipati et al., in Proceedings of the 1993 Polyurethanes World Congress, Society of the Plastics Industries, New York, October 1993, 146-53. ! 4. Performance Test Results for Freezers Containing Vacuum Insulation Panels, H. A. Fine and S. R. Griffin, Proceedings of the International Conference on Alternatives to CFCs and Hdlons, FGU, Berlin, Germany, 1992, 317-22. ! I I I 5. Test Results for Refrigerator/Freezers Containing Vacuum Insulation Panels, H. A. Fine, G. J. Haworth and R. Srikanth, Proceedings of the International Conference on Alternatives to CFCs and Halons, FGU, Berlin, Germany, 1992, 305-15. t i 6. Evaluation of Advanced Insulations for Refrigerators, G. J. Haworth, R, Srikanth, and H. A. Fine, Proceedings of the 44th. Annual International Appliance Technical Conference, Ohio State University, Columbus, Ohio, May 1993, 1-12 7. Development and Application of Vacuum Insulation Technology to Refrigerators, G.A. Mellinger and K. L. Downs, presented at International Conference on CFC and Halon Alternatives, Washington, DC, September 1992. 8. Finite Element Analysis of Heat Transfer Through the Gasket Region of Refrigerator/Freezers, Report Number EPA-430-R-92-009, U.S. Environmental Protection Agency, October 1992. 9. Linear Compressors—A Maturing Technology, N.R. van der Walt and R. Unger, presented at 45th International Appliance Technical Conference, University of Wisconsin, May 1994. 10. "Can a Fancy Plug Cut Energy Costs?," Consumer Reports, November 1993, 694. 11. Experimental Results with Hydrocarbon Mixtures in Domestic Refrigerator/Freezers, B.Y. Lin, M4-L. Tomask and R. Radermacher, paper sumitted to ASHRAE, April 1994. t 12. R22/R152a Mixtures and Cyclopropane (RC 270) as Substitute for R12 in Single-Evaporator Refrigerators: Simulation and Experiments, K. Kim, U. Spindler, D.S. Jung, R. jRadermacher, ASHRAE Trans., Vol. 99, Part 1, Paper #3655. 69 ------- Energy-Efficient Refrigerators 13. Evahiation ofHFC-134a and HFC-152a as Working Fluids in a Domestic Refrigerator/Freezer, J. Pannock, Z. Liu, K. Yu, R. Radermacher, ASHRAE Transactions, Vol. 100, Part 1. 14. Testing of Domestic Two-evaporator Refrigerators with Zeotropic Refrigerant Mixtures, Bob Rose, Dong Soo Jung, R. Radermacher, ASHRAE Transactions 1992, Vol. 98, Pt. 2, Paper #3620. 15. R. Radermacher, "Progress Report to EPA," 1/12/93. 16. An Experimental Study of the Performance of a Dual-Loop Refrigerator/Freezer System, S. Won, D. Jung, R. Radermacher, Submitted to International Journal of Refrigeration. 17. Experimental Research and Development of a Tandem System Domestic Refrigerator, K. Kim, B. Kopko and R. Radermacher, Paper submitted to ASHRAE Transactions. 18. Development and Testing of a High Efficiency Refrigerator, Q. Zhou, J. Pannock, R. Radermacher, ASHRAE Transactions, Vol. 100, Part 1. 70 ------- ------- ------- |