&EPA
                    United States
                    Enviromental Protection
                    Agency
                       Office of Atmospheric
                       and Indoor Air
                       Programs
EPA-430-R-94-011
June 1994
Energy-Efficient Refrigerator
Prototype  Test Results
                                     United Stales   Office o! Atmospheric EPA-430-R-93-OC8
                                     Emiromenlal Projection and Indoor Air  June 1993
                                     Agency     Programs
                                     Multiple Pathways to
                                     Super-Efficient Refrigerators
                                     Uriled Slates  Offico of Atmospheric EPAM30/R-92/OQ9
                                     EfM/wnental Protection andlndoorAir   Odober1992
                                     Agency    Programs

                             S C P A  Finite Element Analysis of Heat
                             \S La r M  Transfer Through the Gasket
                                     Region of Refrigerator / Freezer
                                                                 Recycled/Recyclable
                                                                 Printed with Soy/Canola Ink on paper that
                                                                 contains at least 50% recycled liber

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ACKNOWLEDGMENTS

This report has been compiled by H. Alan Fine and Jean Lupinacci. of the Global Change
Division of the U.S. Environmental Protection Agency and Professor Reinhard
Radermacher of the Center for Environmental Energy Engineering at the University of
Maryland.  The authors wish to thank the many students at the University and
technicians and engineers at the many companies who worked to develop the prototypes
tested in this report.  Particular thanks must go to Admiral Company, Frigidaire
Company, GE Appliances, Haier Group, ShangLing Refrigerator Company, W.C. Wood
Coppany Ltd., and Whirlpool Corporation for their donation of refrigerators and/or
help in the manufacture of the prototypes. Many component suppliers, including
Aladdin Industries, Inc., AMERICOLD, Degussa AG, Owens-Corning, and Thermalux,
are also gratefully acknowledged for their donations and help on this project.

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                                    CONTENTS
                                                                                Page

 Findings	  1

 I. Introduction  	  3

    LA.    Purpose of Report	  4
    I.B.    Energy Test Procedure	  5
    I.C.    ERA Energy Calculations  	  7

 II. Cabinet Modifications  	  9

    II.A.   Foam Insulation Enhancements	  10
           II.A.1.  Thick-Wall Foam Insulation		  10
           II.A.2.  Lower-Thermal Conductivity Foam Insulation—Carbon Black ....  12

    ILB.   Vacuum Insulation  	  14
           II.B.l.  VIP Insulation	  15
                  ILB.l.a.   VIP Insulation—Chest Freezers	  15
                  II.B.l.b.   VIP Insulation—Upright Freezers	  17
                  II.B.l.c.   VIP Insulation—Top-Freezer Refrigerators  	  18
                  II.B.l.d.   VIP Insulation—Side-by-Side Refrigerators	  20
           II.B.2.  Aerogel Insulation	  22
           ILB.3.  Owens-Corning Evacuated Insulation	  24
           II.B.4.  Aladdin Insulation	  26

    II.C.   Improved Gaskets	  27
           II.C.l.  Improved Gasket—VIP  Insulated Refrigerator 	  28

III. Cycle Improvements	  31

    III.A.  Improved Components	  32
           III.A.l. Linear Compressor	  33
           III.A.2. Inverter	  34
           III.A.3. Voltage Regulator	  35
                  III.A.S.a.  Green-Plug—New Top-Freezer Refrigerator 	  35
                  III.A.S.b.  Green-Plug—Side-by-Side Refrigerator	  36
           III.A.4. Hot Water Refrigerator	  37

    III.B.  Improved Refrigerants	  38
           III.B.l. Improved Refrigerants-Hydrocarbon Blends	  38
           III.B.2. Improved Refrigerators—Cyclopropane 	  39
           III.B.3. Improved Refrigerators—HFC-134a and HFC-152a	  40
           III.B.4. Improved Refrigerants—HCFC-22 and HFC-152a Blends	  41
                                           11

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   III.C.    Improved Cycle	 .	:	  42
     I      III.C.1. Lorenz-Meutzner Cycle	  42
                  IILC.l.a.  Lorenz-Meutzner Cycle—Zeotropic Refrigerant Mixtures  42
                  III.C.l.b.  Lorenz-Meutzner Cycle—Hydrocarbon Blends	  43
                  III.C.l.c.  Lorenz-Meutzner Cycle	  45
     ;      III.C.2. Modified Lorenz-Meutzner Cycle	  46
     1             III.C.2.a.  Modified Lorenz-Meutzner Cycle—U.S. Refrigerators  ...  46
     |             III.C.2.b.  Modified Lorenz-Meutzner Cycle—Chinese Refrigerator .  47
     ,      III.C.3. Dual-Loop System	 .  48
           III.C.4. Two-Stage Refrigerator	  50
           m.C.5. Kopko Cycle	|	  51

IV. System and Cabinet Modifications	  59

    ly.A.  Double Insulation and Lorenz-Meutzner Cycle	  60
     I      IV.A.1. Double Insulation	  61
     i      IV.A.2. High-Efficiency Compressor	  61
     ;      IV.A.3. Modified Lorenz-Meutzner Cycle	  62
     !      IV.A.4. Improved Gasket	  63
     I
    ly.B.  Double Insulation and Kopko Cycle 	  64
     i                                                           !
    IV.C.  Double Insulation and Alternate Refrigerants	  67
           IV.C.1. HFC-152a	  67
     i      IV.C.2. Hydrocarbon Mixtures	  68

 V. References	 .  69
                                         in

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                                  TABLES AND FIGURES
                                                                                  Page
    TABLES
   I.I University of Maryland and Manufacturer Test Results	  6

   II. 1 Double-Insulated Refrigerators	  11
   II.2 Carbon-Black Foam Refrigerators	  12
   II.3 Typical Vacuum Insulation Thermal Conductivities	  14
   II.4 VIP Insulated Chest Freezers	  15
   II.5 VIP Insulated Upright Freezers	  17
   II.6 VIP Insulated Top-Freezer Refrigerators  	  18
   II.7 VIP Insulated Side-by-Side Refrigerators	  20
   II.8 Aerogel Insulated Top-Freezer Refrigerators  	  22
   II.9 OC Insulated Top-Freezer Refrigerators	  24
  11.10 Aladdin Insulated Top-Freezer Refrigerators	  26
  11.11 VIP Insulated Refrigerator with Improved Gasket	  28

 III.l  Linear Compressor	  32
 III.2  Inverter	  34
 III.3  Green Plug—New Top-Freezer Refrigerator  	  35
 III.4  Green Plug—Side-by-Side Refrigerator	  36
 III.5  Hot Water Refrigerator	  37
 III.6  Hydrocarbon Blends	7	  38
 III.7  Cyclopropane	  39
 III.8  Minimum Energy Consumption of the Optimized Systems	  40
 III.9  Calorimeter Data for the Two Compressors	  40
111.10  HCFC-22 and HFC-152a Blends	  41
III.ll  Lorenz-Meutzner Cycle—Zeotropic Refrigerant Mixture  	  42
III. 12  Lorenz-Meutzner Cycle—Hydrocarbon Blends  	  43
III. 13  Lorenz-Meutzner Cycle	  45
111.14  Modified Lorenz-Meutzner Cycle—U.S. Refrigerator	  46
111.15  Modified Lorenz-Meutzner Cycle—Chinese Refrigerator	  47
111.16  Dual Loop System	  48
111.17  Two-Stage System	  50
IH.18  Kopko Cycle	  51
111.19  Kopko Cycle—First Modiacation	  52
111.20  Kopko Cycle—First Modification Test Results	  53
111.21  Kopko Cycle—Second Modification	  54
111.22  Kopko Cycle—Second Modification Test Results	  55
111.23  Kopko Cycle—Third Modification and Test Results	  56
111.24  Kopko Cycle—Fourth Modification and Test Results	  57
                                            IV

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I V.I   Double-Insulated, Lorenz-Cycle Refrigerator	
IV.2   High-Efficiency Compressor 	
IV.3   Modified Lorenz-Meutzner Cycle  	
IV.4   Double-Insulated, Kopko-Cycle Refrigerator	
IV.5   Specifications for the First Modification	
IV.6   Test Result for the First Modification	
IV. 7   Compressor Comparison for Kopko Modifications  .
IV.8   Increased Insulation with Refrigerant HFC-152a . . .
IV.9   Increased Insulation with Hydrocarbon Refrigerants
60
61
62
64
65
66
66
67
68
   FIGURES

 11.1  Cross Section of Gasket Region
 II.2  Front View of Gasket Region . .
29
30
I V.I  Schematic Representation of Improved Gasket	  63

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VI

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                                                                  Prototype Test, Results
                                                                          May 1994
                                   FINDINGS
Working prototype refrigerator/freezers demonstrating a wide variety of existing and
emerging technologies for energy conservation have been built and tested.

Energy-efficiency gains resulting  from improvements to individual components can be
grouped as follows:
n




o Energy Reduction
5-10
10-15
15-20
25-30
, Improvement
improved gasket region design
inverter
hydrocarbon refrigerants
50% coverage advanced insulation
linear compressor
Lorenz cycle in side-by-side R/F
Lorenz cycle in top-freezer R/F
Kopko Cycle
Adding 1.5 inches of foam insulation
Substantial energy-efficiency gains resulting from a combination of improvements can be
grouped as follows:
% Energy Reduction
30-40
40-50
>50
Improvements
Adding 1.5 inches of insulation and Kopko cycle
Adding 1.5 inches of insulation, better compressor, Lorenz
cycle, and improved gasket
Adding insulation, better compressor, and HFC-152a
refrigerant to a Chinese R/F
Adding insulation, better compressor, and hydrocarbon
refrigerants to a Chinese R/F
The EPA Refrigerator Analysis (ERA) model predictions agree with measurements made
on the prototypes.

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Energy-Efficient Refrigerators

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                                                                   Prototype Test Results
                                                                            May 1994
I. INTRODUCTION
Many factors have driven industry to implement energy-efficiency improvements in
household refrigerator/freezers (R/Fs).  The 1993 DOE Energy Efficiency Standards have
been in effect for a little more than one year, and many manufacturers have models on
the market that exceed this standard. In fact, the winner of The Golden Carrot
Competition for $30 million, Whirlpool Corporation, will be selling R/Fs in 1994 that
exceed the standard by more than 25 percent, without using ozone-depleting CFCs.
Other manufacturers are expected to offer similar energy efficient products in the near
future.

There appears to be  dramatic changes occurring in consumer buying preferences.
Consumer acceptability is an important factor to selling refrigerators.  Based on the
marketing perception that consumers are only first cost driven and place high value on
internal volume, manufacturers were reluctant to explore cost-effective design changes to
increase energy efficiency, particularly by adding more insulation to the refrigerator
walls.

The recent success of Sears's program to prominently market the "Energy Efficient" 1993
moldels may change  the idea that energy efficiency would not drive the sale of
refrigerators. The Sears program consisted of training, advertising, point-of-sale
identification, and charts that helped customers understand the substantial savings and
environmental benefits from purchasing energy-efficient refrigerators. Early indications
from  Sears showed that many customers would ask for the new models and were even
willing to wait  and pay more for them.

There is not just one path or design approach that leads to super-efficient refrigerators
but rather multiple pathways to achieve large energy savings. Each refrigerator
manufacturer will decide on the most cost-effective set of options emd technologies based
on tits current products' energy efficiency, design, size class, cost-structure, and other
factors.

In evaluating the potential energy savings in R/Fs, EPA has conducted a wide variety of
analyses, including technical evaluations, model  development and analysis, cost analyses,
marketing and  consumer preference analysis, and prototype development and testing.
All are necessary to determine the ultimate acceptability of the various options.
Manufacturers will conduct similar analyses pertaining to their own product lines and
circumstances as they commercialize new energy-efficient products.

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Energy-Efficient Refrigerators
LA PURPOSE OF REPORT
This report will summarize the test results for the numerous R/Fs built by EPA and our
partners to evaluate a wide variety of technologies to increase energy efficiency and to
eliminate the use of CFCs.  The results for many of the prototypes represent the joint
efforts of EPA, the University of Maryland, and various equipment and refrigerator
manufacturers.  In many cases, the prototypes were tested at both the University and  the
individual companies.  The partnerships were a critical component of the success of the
prototypes.  The interaction between the various experts was useful to define realistic
parameters, resolve problems, and make modifications to the prototypes on the
production line.

The prototypes were developed to test technologies that increase energy efficiency and
eliminate CFCs.  The refrigerators that were built and tested are not meant to showcase
all combinations of technologies, but rather to demonstrate significant energy savings
that could be achieved with existing and emerging technologies.

Some of the prototypes were built to test the performance of a single  technology.  Other
prototypes combined technologies that demonstrated substantial energy savings to
identify any interactive effects between the different  technologies and different systems.

The report is divided into four sections.

•  The Introduction describes the  purpose of the report, the  testing methodology, and
   comparison with ERA energy calculations.

•  The Cabinet Improvements section summarizes the test results from refrigerator/
   freezers that demonstrate improvements to the thermal envelope of the unit.

•  The Cycle Improvements section summarizes the test results from refrigerator/freezers
   that demonstrate improved components, alternate refrigerants, and alternate cycles.

•  The System and Cabinet Modifications section provides a summary of test results
   from units that  combined both  improvements to the cycle and the  cabinet.

Many technologies have shown great promise for future development, but further
evaluation will need to be conducted for commercialization.  Continued applied research,
manufacturability, long-term reliability, and cost analyses may be required by the
manufacturers.

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                                                                  Prototype Test Results
                                                                           May 1994
I.B  ENERGY TEST PROCEDURE
Except as noted, refrigerator energy tests were performed at the University of Maryland
(Ul Md.) according to the DOE test procedure, with some minor modifications.  The
modifications were necessary to arrive at well optimized refrigeration cycles in a short
period of time.  For those tests that included a defrost cycle and the anti-sweat heaters,
the outcome is the same as for the DOE procedure.

During testing at U. Md., all compartment temperatures and the room temperature are
measured and maintained as prescribed by DOE.  The compartment temperatures,
however, are maintained with an independent temperature controller, not the original
refrigerator thermostat.  Generally, the temperature controller controls the freezer
temperature, while the food compartment temperature is adjusted by either a second
controller (Kopko and dual loop systems) or by adjusting charge and capillary tube
length.  The instantaneous power and energy consumption are measured with watt and
watt-hour transducers, respectively.
   i
The defrost is normally deactivated during testing at U. Md. and tests are conducted for
one day  (24h).  The system, however, is defrosted regularly to maintain system
performance. When a defrost cycle is included in the measurement at U. Md., the energy
consumption is measured from the onset of one defrost cycle to the onset of the next.
The energy consumption is then extrapolated to 24h.  When defrost cycles and anti-sweat
heaters in the on and off positions are included, the U. Md. method is the same as the
DOE method, except it is faster and more accurate. The refrigerator performance is
determined at a freezer temperature of 5°F rather than measuring above and below this
temperature and then interpolating to it.

Modifications to the defrost cycle were not tested. In certain instances, such as the
incorporation of either the Lorenz or  Kopko  cycle into the R/F, additional energy savings
could be achieved by modifying the defrost cycle.

Table LI reports refrigerator tests that were repeatable within ±1 percent when repeated
under the same conditions and at the same laboratory, and within +. 5 percent when
compared to other laboratories.  The table also shows a comparison of the U. Md. test
results and the test results of the manufacturers conducted according to the DOE
standard.

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Energy-Efficient Refrigerators
            Table I.I University of Maryland and Manufacturer Test Results
: : . -• Energy !
Test Location land FF Temperature I|Z Temperature Consumption ;
ModeJ Tested Conditions • (°F) . (°F) (kWh/24h) ;
t ; • i
Admiral
RB19xx
with vacuum
insulation
Whirlpool
ET20ZK
Thick-wall 20
ft3 Whirlpool
U. Md. w/o defrost
U. Md. with defrost
Admiral DOE Test
U. Md. with anti-sweat
heaters on
Whirlpool with anti-
sweat heaters on
U. Md. with anti-sweat
heaters on
Whirlpool with anti-
sweat heaters on
U. Md. with anti-sweat
heaters off
Whirlpool with anti-
sweat heaters off
5.3
4.9
5
5.0
5.0
5.0
5.0
5.0
5.0
38.5
38.3
38
41.9
40.0
37.4
38.1
37.1
36.6
1.96
2.16
2.12
2.17
2.31
1.91
1.85
1.38
1.44

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                                                                 Prototype Test Results
                                                                          May 1994
I.C ERA ENERGY CALCULATIONS
The EPA Refrigerator Analysis (ERA) computer model can be used to estimate the
impact on energy consumption of a wide variety of modifications to the refrigerator
cabinet and components. ERA predicts the performance (energy consumption) of
household R/Fs and is capable of simulating various cabinet, auxiliary, and cycle
configurations.  It consists of four major components:

1.  j^. menu-driven input processor;

2.  Estimation of the cabinet loads;

3.  Thermodynamic cycle simulation; and
   i
4.  Energy-consumption calculations.
   I                                                          ;
Additional details are provided in the ERA User's Manual. [1]

The results of a variety of ERA calculations have been presented in. Multiple Pathways to
Super-Efficient Refrigerators. [2]  These results have been compared to the test results of
applicable prototype models.

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Energy-Efficient Refrigerators
8

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                                                                Prototype Test Results
                                                                         May 1994
II. i CABINET MODIFICATIONS
A series of prototype refrigerator/freezers (R/Fs) were produced that contained
improvements to the thermal envelope of the units. These improvements included:

• Improvements to the foam insulation system,

• The addition of vacuum insulation, and/or
   i

• Improvements to the gasket system.
   l
Details of the prototypes and the resulting energy savings are presented in the following
section.

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Energy-Efficient Refrigerators
II.A  FOAM INSULATION ENHANCEMENTS
The overall thermal performance of the cabinets was improved by increasing the
thickness of the R/F cabinet or by reducing the thermal conductivity of the foam., The
results of these tests are described next.       ••>•.,
II.A.1  Thick-Wall Foam Insulation
Polyurethane foam insulation was added to the walls of a refrigerator to reduce heat:
flow into the refrigerated volume. The internal volume was maintained by adding the
insulation to the exterior of the. unit, at the expense of slightly larger exterior dimensions.
Alternatively, insulation can be added to the interior surfaces, but at the expense of
internal volume.
Baseline Unit
The baseline unit was a standard 20 ft3 automatic-defrost top-freezer
refrigerator, Whirlpool model number ET20DK.  Dimensions and
daily energy consumption are presented in Table 11.1.
Thick-Wall Unit  The "double-insulated" refrigerator was manufactured by installing
                  the liner for the" standard 20 ft3 model into the shell of a standard
                  25 ft3 unit, model ET25DK.  The unit was then foamed and completed
                  with components identical to those for the standard ET20DK. Special
                  doors did, however, have to be manufactured to fit the unit.

                  Two units were built and tested at Whirlpool.
10


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                                                                  Prototype Test Results
                                                                           May 1994
                      Table H.l Double-Insulated Refrigerators
Baseline Thick- Wall
Unit Unit
Volume (ft3)

Freezer
Fresh Food
Exterior Dimensions (in)
Height
Width
Depth
Insulation Thickness (in)
Doors
FF Sides
FF Back
FF Bottom
FZ Sides
FZBack
FZTop
Mullion
Energy Consumption Whirlpool
(kWh/24h) U.Md.
EPA-RTP

5.5
14.4


66
32
28

1.5
1.8
1.8
1.8
•2.2
2.2
2.2
2.5
2.33


5.5
14.4


69
35
31

2.8
3.3
3.6
3.3
3.6
4.0
3.6
2.5
1.63 + 0.03
1.73
1.72
Discussion   As can be seen from the above table, approximately 1.5 inches of foam
   •          were added to all exterior surfaces of trie unit. Interior volume was
   i          maintained, while exterior dimensions were increased by 3 inches on each
   i          dimension.
             A measured 27 percent decrease in energy consumption was achieved. The
             ERA model predicts a 19 percent energy reduction for the addition of
             1 inch of insulation to the exterior of 18 ft3 R/Fs and 29 percent for the
             addition of 2 inches. ,[2]  ERA is thus in good agreement with the
             measurements.
                                                                                 11

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Energy-Efficient Refrigerators
II.A.2  Lower Thermal Conductivity Foam Insulation—Carbon Black
The thermal performance of foam insulation is a complex function of three modes of heat
transfer that occur within the insulation: heat conduction in the solid and vapor phases
and thermal radiation through the composite.  Reducing the amount of heat transferred
by any of these mechanisms should reduce the thermal conductivity of the foam and the
rate of heat flow through the foam for a given set of conditions.

The addition of carbon black particles to polyurethane foam reduces thermal radiation
transport and the thermal conductivity of the foam. Black foams have been developed
for the construction industry and are under development for appliance applications by
Miles Inc. and the Center for Applied Energy Research Inc.  [3]
Baseline Unit
Black-Foam
Units
The baseline model was a standard 17 ft3 automatic-defrost top-freezer
model, Admiral Co. model number RB17OPW. Foaming of pre-
assembled empty cabinets with an HCFC-141b-blown foam was done at
Miles Inc. The foam formulation was developed by Miles for this trial.
After foaming, the units were returned to Admiral for final build-up and
testing.  Foam properties and energy test results are shown in
Table 11.2. [3]

Foam with the same formulation but containing 6.3 percent carbon black
was used for these units.  All other processing and  testing protocols
were identical.

      Table IL.1 Carbon-Black Foam Refrigerators
i ' i ' 1 Baseline Black-Foam
" ' ; Units ! Units .
• : ; : -:1 " • : -. , - -r ! r
Foam Thermal Conductivity
(BTU*in/(h*ft?*0F))
Foam Density (Ib/ft3)
Energy Consumption (kWh/24h)
0.129
1.75
1.84 + 0.03
0.12
1.87
1.83 + 0.01
Discussion     The thermal conductivity of the carbon-black loaded foam was eight
               percent lower than the baseline HCFC-141b foam. Computer model
               simulations made by Admiral predicted a 3.2 percent lower energy
               consumption for the refrigerator. ERA predictions for 18 ft3 models [2]
               show energy reductions ranging from 3.4 to 4.3 percent with an average
               of 4.0 percent.
 12

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                                                  Prototype Test Results
                                                          May 1994
The actual energy consumption of the black-foam prototype refrigerator
was less than one percent lower than the baseline. Tests, including
reverse heat flow measurements, are being performed to determine why
larger energy savings were not observed. One hypothesis for why the
eight percent  lower thermal conductivity black-foam did not reduce the
energy consumption of the unit was that the black-foam units were
made in February 1993 and the baseline models in May. Small
improvements in components over this period may have lowered the
energy consumption of the baseline models and masked the effect of the
improved foam.
                                                                13

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Energy-Efficient Refrigerators
II.B  VACUUM INSULATION
A number of advanced insulation systems are currently under development.  These
systems generally consist of a filler material contained in a gas-tight barrier. All of the
concepts, except for gas-filled panels, attain their lower thermal conductivity at reduced
pressure (under vacuum).  Filler materials incorporated into these advanced insulations
include ceramic spacers,  precipitated silica or other powders, fiberglass, aerogel tiles, and
open-cell foams.  Barrier materials range from laminated polymer structures to stainless
steel.

High thermal resistance (low thermal conductivity) elements can be combined with foam
insulation in the walls of R/Fs to improve their thermal performance, without effecting
their structural integrity. Four types of advanced insulation systems were tested in R/Fs
and/or freezers.  Typical center-of-panel properties for the vacuum insulations employed
in the prototypes are summarized in Table II.3.  It is important to note that the
conductivities of panels used in the prototypes may be substantially higher than those
given in the table, as edge  effects may substantially change the thermal performance of
small panels, especially those fabricated with metallic barriers.

             Table II.3 Typical Vacuum Insulation Thermal Conductivities
* 1 ; :' 1 ' : ; '
; : ! Thermal Conductivity ;
Description \ ' Manufacturer (BTU*in/(h*ft2*°F)) 1
• • i . - i
Precipitated Silica in Plastic
Laminate (VIPs)
Aerogel Tiles in Plastic Laminate
Fiberglass in Stainless Steel
Precipitated Silica and Carbon
Black in Stainless Steel
Degussa AG
Thermalux
Owens-Corning
Aladdin Industries, Inc.
0.050 ±0.0031
0.051+ 0.0011
0.018 + 0.0022
0.0421
 Measurements made by Materials Thermal Analyses Group at Oak Ridge National Laboratory.
1 Measurements made by Owens-Corning.
14

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                                                                   Prototype Test Results
                                                                            May 1994
II.B.1. VIP Insulation
  j
WB.l.a VIP Insulation—Chest Freezers

Vacuum insulation panels (VIPs) consisting of precipitated silica filler in a plastic-
laminate barrier/container were installed in three chest freezers at W. C. Wood Co. Ltd.
injNovember 1991. The balance of the composite insulation system consisted of W. C.
Wood's standard foam formulation blown with CFC-11.

Baseline Units  Two production model chest freezers were employed as baseline units:
  i              WC42-xx and WE46-xx.  Storage capacity, insulation thickness, and
  ;              energy consumption data for these models are listed in Table II.4.
  \
VIP Units       VIPs were mounted on styrofoam inserts adjacent to the cold-wall
  I              evaporators on the sides and bottom of the three prototype units.  The
  i              cabinets were then assembled, foamed, and built-up on the production
  }              line without any additional modifications.  The percentages of area
  i              covered by VIPs and energy consumption results are presented in the
  j              following table. Additional details on panel sizes and locations are
  i              available in reference [4].
  i                                  '                          I
  i
                        Table HA VIP Insulated Chest Freezers
WC42-XX
• ; . ' ; ; #1
Capacity (ft3)
Insulation Thickness (in)
Baseline Energy Consumption
(kWh/24h)
% Area Covered by VIPs
Energy Consumption (kWh/24h)
% Energy Reduction
14.8
2.5
1.16
54
1.04
11
WC42-Jx ; WE46-XX
•U.1

14.8
2.5
1.16
54
0.99
15
16.5
3.0
1.24
44
1.08
13
Discussion     An average 13 percent reduction in energy consumption for an average
  I             50 percent area of coverage was obtained.  The baseline models were
  i             relatively high-efficiency models incorporating thick insulation walls.
  j             The impact of VIPs on energy consumption would thus be less than that
  1             for freezers or R/Fs with thinner walls.
                                                                                  15

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Energy-Efficient Refrigerators
               Measurements performed, on the WC42-xx units approximately 18
               months after production showed 13 and 16 percent increases in energy
               consumption with 12 and. 7 percent increases in run time for units 1 and
               2, respectively. The increase for unit one is much higher than that
               which would be expected from the aging of the foam alone.  Either a
               panel failure or aging of the panels must have occurred. The increase in
               run time for unit two would be consistent with foam aging.  The
               significant increase in energy consumption, as compared to the increase
               in run time, has not been explained.
16

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                                                                  Prototype Test Results
                                                                            May 1994
II.B.l.b VIP Insulation—Upright Freezers

VIPs were installed in upright freezers at W. G. Wood Co. Ltd. in February 1992. The
balance of the composite insulation system consisted of W. C. Wood's standard CFC-11
blown foam insulation formulation, with the exception of fiberglass doors.

Baseline Units Two production model  upright freezers were used as baseline models:
               WVF47-xx and WV58-xx,  Data on these models are presented in
               Table 71.5.

Vllf Units      VIPs were mounted on  the sides, back, and top of the smaller unit and
   !            on the sides, back, top,  and bottom, of the larger model.  Cabinets were
   I            then assembled, foamed, and built-up on the production line without
   j            any other modifications. Percentages of area covered and test results
               follow. Additional details on panel sizes and locations can be found in
               reference [4].

                       Table IL5 VIP Insulated Upright Freezers
_ • . " ' : : . WVF47-XX . WV58-xx
Capacity (ft3)
Insulation Thickness, (in)
Baseline Energy Consumption (kWh/24h)
% Area Covered by VIPs
Energy Consumption (kWh/24h)
% Energy Reduction
16.7
2.5
2.15 ,
56 '
2.02
6
20.3
2
•2.34 ,-=.-:
53 .
2.05
12
Discussion     The approximately 10 percent energy reduction is lower than that
               achieved for the chest freezers even though the walls are thinner.  This
               probably results from the fiberglass insulated door, which allow a
               disproportionate amount of heat to flow into the cabinet.

               Retests on the prototypes performed approximately 14 months after
               production showed a 5 percent increase in energy consumption and
               compressor run time. This is consistent with aging of the foam
               insulation, alone/over this period.
                                                                                 17

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Energy-Efficient Refrigerators
IJ.B.2.C VIP Insulation—Top-Freezer Refrigerators

VIPs were installed in 19 ft3 automatic-defrost top-freezer refrigerators produced by the
Admiral Company in 1991 and 1992. The balance of the insulation system was either
Admiral's standard foam formulation blown with CFC-11 or a special CO2-blown
formulation.

Baseline Units The 1991 baseline units were standard Model RB19xx production units
               built during the last quarter of the year. The 1992 baseline models were
               RB19K2A production models, modified with a flat back to accommodate
               larger VIPs. Foam insulated doors also replaced the standard fiberglass
               insulation in all baseline  models.  DOE energy test results for the
               various units are presented in Table 11.6.

VIP Units      VIPs were mounted on the sides and top adjacent to the steel cabinet
               and on the back adjacent to the plastic liner on all prototype units.
               Panels were also mounted adjacent to the steel cabinet bottom on the
               1992 units. Cabinets were then assembled,  foamed, and built-up without
               any additional modifications. Three sets of cabinets and doors were
               generally produced. These components were tested together or in
               combination with doors or cabinets from the baseline models to generate
               the data presented below. Additional information on the panel sizes
               and locations can be found in references [5] and [6}.

                  Table 11.6 VIP Insulated Top-Freezer Refrigerators
\ : ! ' - " 1 : : -1 ..---.
Year ; 1991 j 1992 1992
Foam Blowing Agent
Baseline DOE Energy Consumption
(kWh/24h)
VIPs in Cabinet and Doors
% Area
DOE Energy
% Reduction
VIPS in Cabinet only
DOE Energy
% Reduction
VIPs in Doors Only
DOE Energy
% Reduction
CFC-11
2.36 + 0.12

47
2.12 + 0.05
10

2.27 + 0.06
4

2.23 + 0.07
5
CFC-11
2.26 + 0.06

68
2.08 + 0.06
8

2.15 + 0.06
5

2.21 + 0.01
2
C02
2.58 + 0.10

68
2.26 + 0.09
13




18

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                                                                  Prototype Test Results
                                                                           May 1994
Discussion     The energy reduction results for the 1992 prototypes were less than
  i             expected. The results for the units made with CFC-11 foam are based
               on only two sets of cabinets and doors.  Two additional sets were made
  |             but found to have very poor energy performance. These units were
  I             disassembled after testing and found to have punctured panels.  The
  i             percentage reduction for the poorer insulating CO2-blown foam was as
  '             expected. Measurements were not made for the cabinet-only and door-
  1             only configurations, as rapid aging of these foams would have produced
  '             confusing results.

  I             The average 10 percent energy reduction is smaller than the 14 to 16
               percent predicted by ERA for 50 percent area of coverage of several
  !             18 ft3 refrigerators. [2] The ERA calculations were based on 1-inch thick
  '             panels, while the tests were performed with 0.5- and 0.75-inch thick
  '             panels. Linear extrapolation of the test results for the 1991 prototypes to
               1-inch thick panels yields a 14 percent energy reduction.  Similar
  i             calculations  for the  1992 prototypes yields  12 and 19 percent reductions
               for the CFC-11 and CO2 foams, respectively. Only the results for the
  i             1992 prototypes with CFC-11 foam are not in good agreement with ERA.
               As mentioned previously, there may have been problems with
  ;             punctured panels in these tests.
                                                                                19

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Energy-Efficient Refrigerators
ILB.l.d VIP Insulation—Side-by-Side Refrigerators

A set of 22 ft3 side-by-side refrigerators were built at Admiral Co. in 1991. The insulation
system in these units consisted of VIPs and Admiral's standard CFC-11 foam
formulation.

Baseline Units The baseline units were standard production models built in late 1991,
               model CNS22V8A. All walls and doors of the baseline units contained
               foam insulation.

VIP Units     VIPs were mounted on the top, sides, and doors of the prototype units.
               All panels were attached to the steel case, except the back panels that
               were attached to the liner. Cabinets were then assembled, foamed, and
               completed without any additional modifications on the production line.
               Additional details on panel sizes and location can be found in reference
               [5]. Test data are presented in the following table.

                  Table IL7 VIP Insulated Side-by-Side Refrigerators
             Baseline DOE Energy Consumption (kWh/24h)
2.98 + 0.08
             VIPs in Cabinet and Doors

               % Area Covered by VIPs
               DOE Energy
               % Energy Reduction
    49
2.96 ± 0.07
    1
             VIPS in Cabinet only

               DOE Energy
               % Energy Reduction
2.82 ± 0.07
    5
             VIPs in Doors Only

               DOE Energy
               % Energy Reduction
3.06 + 0.15
    -3
Discussion   The presence of the VIPs in the long slender doors of the side-by-side units
             resulted in warpage and poor sealing.  Thus the energy consumption went
             up for the doors-only case and only went down one percent for the cabinet
             and doors case. Foam voids were also observed in the cabinet.  These were
             patched prior to energy testing but may have contributed to the small
             reduction in energy that resulted for the cabinet-only tests.
20

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                                                       Prototype Test Results
                                                                May 1994
Similar vacuum panels at approximately 55 percent area of coverage have
been installed in a 25 ft3 side-by-side model. [7]  These panels resulted in a
17 percent reduction in energy consumption.
                                                                     21

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Energy-Efficient Refrigerators
II.6.2 Aerogel Insulation

Panels consisting of aerogel tiles encapsulated in a plastic laminate barrier/container
were installed in top-freezer automatic-defrost refrigerators. The panels were
manufactured by Thermalux from 12 in. by 12 in. by 0.5 in. silica aerogel tiles, which
were cut and assembled into the desired panel sizes. The refrigerators were made at
Admiral Co., and the remainder of the insulation composite was their standard foam
formulation blown with CFC-11.

Baseline Units  The baseline units were standard Admiral production models
                manufactured in 1992, model RB19K2A. Several indentations in the
                backs of the units were  eliminated to allow a higher coverage of vacuum
                panels. Foam-insulated doors were also used to replace the standard
                fiberglass insulation.  All other  dimensions and components were
                unchanged from the standard production models.

Aerogel Units   Three prototype units containing aerogel panels were fabricated.
                Aerogel panels were attached to all surfaces of the prototypes, including
                the bottom. All panels except those on the back were attached to the
                steel case.  The panels were 1-inch thick, except those on the fresh food
                compartment sides, bottom, and back, which were 0.5 inches thick. The
                units were assembled, foamed,  and completed on the normal production
                line without any additional modifications. Additional details on panel
                sizes and locations can be found in reference [6]. Test results follow.

                 Table II.8 Aerogel Insulated Top-Freezer Refrigerators
Baseline DOE Energy Consumption (kWh/24h)
Panels in Cabinet and Doors
% Area Covered by Aerogel
DOE Energy
% Energy Reduction
Panels in Cabinet only
DOE Energy
% Energy Reduction
Panels in Doors Only
DOE Energy
% Energy Reduction
2.26 + 0.06
67
2.10 + 0.09
7
2.12 + 0.07
6
2.24 + 0.05
1
22

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                                                                  Prototype Test Results
                                                                           May 1994
Discussion     The aerogel panels were very fragile, and several were broken during
  i             shipment.  After energy testing, one prototype was disassembled and
  !             also found to have panels that had lost their vacuum.  The panels
  j             located on the bottom of the units also blocked foam flow, resulting in
  ;             voids that had to be patched.  These two problems account for the poor
               performance of these prototypes.

  |             Additional tests of this insulation are not currently possible, as
  •             Thermalux has gone out of business, and they were  the only known
  ;             supplier of large aerogel tiles.
                                                                                23

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Energy-Efficient Refrigerators
II.B.3 Owens-Corning Evacuated Insulation
Vacuum panels consisting of fiberglass in a stainless steel container are produced by
Owens-Corning (OC). As noted earlier, these panels may have center-of-panels thermal
resistivities higher than 50 h*ft2*°F/(BTU*in), but edge effects may substantially lower
their performance in refrigerators.

Baseline Units Baseline units were 1992 Admiral RB19K2A models with flat backs and
               foamed doors as described in section II.B.l.c.

OC Units      Four prototypes were built with OC panels.  Panels were 0.75  inches
               thick, except for the fresh food back, which was 0.5 inches thick.  Small
               panels were used in two of the  prototypes to cover the machine
               compartment. All four units had panels on the other five sides. After
               mounting the panels,  the cabinets were assembled, foamed with
               Admiral's standard CFC-11 foam formulation, and completed  on the
               production line. Test results follow.

                   Table II.9 OC Insulated Top-Freezer Refrigerators
             Baseline DOE Energy Consumption (kWh/24h)
             Panels in Cabinet and Doors

                % Area Covered
                DOE Energy
                % Energy Reduction
             Panels in Cabinet only

                DOE Energy
                % Energy Reduction
             Panels in Doors Only

                DOE Energy
                % Energy Reduction
2.26 + 0.06
    69
1.92 + 0.05
    15
1.99 + 0.05
    12
2.18 ± 0.04
    4
Discussion     The energy reduction results were the best of the advanced insulations
                tested.  This is probably reflective of the higher thermal resistances of
                the panels, measured by Owens-Corning to average almost R-40 per inch
                including edge effects.

                The two units with panels over the machine compartments did not have
                significantly different energy consumption than those without these
24

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                                                   Prototype Test Results
                                                            May 1994
panels.  This is indicative of the fact that small panels will not have an
improved performance over foam, especially for panels with metallic
edges.                 ,

One unit was also known to have a panel that had lost its vacuum.
Again, the performance was not significantly different than that of the
other units.  This is probably indicative of the small number  of
prototypes and the variability in the other components of the refrigerator
masking the effect of one bad panel.
                                                                 25

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Energy-Efficient Refrigerators
II.B.4 Aladdin Insulation
Evacuated panels containing a blend of precipitated silica and carbon black contained in
stainless steel are produced by Aladdin Industries. These panels have slightly higher
center-of-panel thermal resistance than the panels contained in plastic, but edge effects
may substantially lower their effectiveness.

Baseline Units  The baseline models were 1993 RB193PW refrigerators produced by
                Admiral. The only modification to the standard units was the use of
                2-inch thick doors. At the request of Admiral, only percentage changes
                from the baseline are presented in this report.

Aladdin Units  Three prototype units were built with Aladdin panels. All panels were
                1-inch thick, except for 0.5 in. panels on the fresh food back.  Panels
                were not placed over the machine compartment.  Except for the panels
                and 2-inch thick doors, the prototypes were identical to standard
                production models.  Foam blown with CFC-11 was used for the balance
                of the insulation system. [6]

                 Table 11.10 Aladdin Insulated Top-Freezer Refrigerators
Baseline DOE Energy Consumption
Panels in Cabinet and Doors
% Area Covered
% Energy Reduction
Panels in Cabinet only
% Energy Reduction
100%
57
6
5
 Discussion     The Aladdin panels had approximately 15 percent higher areas of
                coverage and 25 percent higher center-of-panel thermal resistances than
                the panels contained in plastic. The energy reductions were, however,
                lower. Edge effects are clearly very important.  Higher center-of-panel
                thermal resistances and larger panels can overcome this problem, as
                demonstrated by the Owens-Corning insulation results.

 26

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                                                                   Prototype Test Results
                                                                            May 1994
ILC Improved Gaskets
Heat flow through the gasket region of the cabinet contributes significantly to the total
load.  Finite element analysis (PEA) of this region of the refrigerator cabinet has shown
that heat flow in this region can be reduced by 50 percent by minor changes to the
design of the flanges on the door and cabinet. [8] Test results for two prototype units
with gasket modifications are presented in the next section and section IV.A.
                                                                                  27

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Energy-Efficient Refrigerators
II.C.1  Improved Gasket—VIP Insulated Refrigerator
Heat flow in the gasket region occurs by conduction down the flanges and then by
convection from the ends of the flanges and the gasket.  Replacing a portion of the
flanges on the inside of the refrigerator with plastic can reduce the total amount of heat
flow in this region by one-half.  In many cases, the cabinet flange does not extend into
the cabinet as far as the gasket.  Unless the small gap between the gasket and interior
liner is sealed, convection from the end of the flange will still occur as if the flange
extended into the refrigerated volume.

Baseline Unit  One of the Admiral RG19xx prototype units built in 1991  and containing
               VIPs was used in this test program (see II.B.l.c.). The energy tests were
               performed at U. Md. with the anti-sweet heaters off (one portion of the
               standard DOE test).

Modified Unit A cross section of the gasket region is shown in Figure ILL The cabinet
               flange was modified by adding a piece of foam insulating tape adjacent
               to the flange on the inside of the refrigerated volume. The door flange
               was modified by removing  the metal that protruded through the flange
               region. A front view of these modifications is shown in Figure 11.2.

             Table 11.11 VIP Insulated Refrigerator with Improved Gasket
Baseline Energy Consumption (kWh/24h)
Energy consumption with door flange modification
% Reduction
Energy consumption with both flanges modified
% Reduction
2.18 + 0.02
2.11
3
2.01 + 0.01
8
Discussion     Slightly greater energy reductions could be achieved by redesigning the
               door flange, as opposed to removing the flange from between the screw
               holes.

               ERA predicted energy reduction of 7 and 11 percent for 25 percent and
               50 percent reductions in heat flow through the gasket region,
               respectively.  The FEA results indicate that an approximately 40 percent
               reduction in heat flow should have occurred, with the modifications
               performed. Thus agreement between ERA and the test results is very
               good.
28

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                                                                  Prototype Test Results
                                                                           May 1994
                    Figure II.l Cross Section of Gasket Region
                                              Door
   Door Flange
                                     Foam Insulation
Cabinet Flange
                                     Gasket
Removal Metal
Insulating Tape
                                 Foam
                                                        Inner
                                                                                 29

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Energy-Efficient Refrigerators
                           Figure 11.2 Front View of Gasket Region
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30

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                                                                 Prototype Test Results
                                                                          May 1994
III.  Cycle Improvements
  t
  i
Aj series of prototype refrigerators was also produced with improved cycle components.
Improvements included:

• i Improved components,                                     i

• Alternate refrigerants, and
  i
• j Alternate cycles.

The results of tests on these prototypes are presented in this section.
                                                                               31

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Energy-Efficient Refrigerators
III.A.  IMPROVED COMPONENTS

III.A.l  Linear Compressor
A linear compressor differs from a conventional reciprocating compressor in that the
motor drives the piston directly. This feature eliminates the crank mechanism and
simplifies the design.  In the linear compressor developed by SunPower Inc.,  gas
bearings guide the piston as it resonates on a spring.  Use of gas bearings and
elimination of the crank greatly reduces friction losses and eliminates the need for
lubricating oil.  The resonant piston reduces motor size and improves motor efficiency.
Reducing the input voltage to the linear motor reduces the stroke of the piston and
allows for easy capacity control. The net result of these improvements  is a simple,
efficient, oil-free, variable-capacity design.  Compressor calorimeter tests with the
SunPower compressor have shown a 15 percent improvement in design efficiency
compared to a conventional reciprocating design. [9]
Baseline Unit
The baseline unit was an 18.6 ft3 top-freezer automatic-defrost
refrigerator produced by Frigidaire, model number FPGS19TSWO.
Prototype Unit The compressor was replaced with the linear compressor. The capillary
               tube and refrigerant charge were optimized for minimum energy
               consumption. Thermocouples were installed.  The remainder of the
               baseline unit remained unchanged.

                            Table 111.1 Linear Compressor
••..'<:• .1 • . 1- T. • • .!.
:i ; Linear .
\ Baseline , Compressor
1 • ! I1' r . ! "
Compressor EER
Charge (g)
Energy Consumption (kWh/24h)
FF/FZ Temperature (°F)
Duty Cycle
% Energy Reduction
5.5
156
1.94
45.2/4.6
0.52

6.2
200
1.73
46.1/4.4
0.48
11
32

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                                                                  Prototype Test Results
                                                                           May 1994
Discussion
The linear compressor was more efficient than the original compressor
and produced an 11 percent energy savings.  The savings were smaller
than expected when compared on an HER basis because the fans also
consume electricity.

ERA predicted a 10 percent energy savings when the linear compressor
replaced a 6.0 EER reciprocating compressor in an 18 ft3 R/F.  [2] The
linear compressor in the ERA analysis was assumed to have an EER of
6.5  and variable capacity control. The test did not include capacity
control, and the linear compressor had an EER of 6.2 and replaced the
Frigidaire unit, which had a 5.5 EER.
                                                                                33

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Energy-Efficient Refrigerators
III.A.2 Inverter
An inverter is a variable-frequency power source that can be used to vary the speed of
electric motors. The inverter used in the experiments is a proprietary design.  It works
with conventional permanent split capacitor (psc) motors such as those used in
refrigerator compressors.
Baseline Unit
The baseline unit was an 18 ft3 top-freezer automatic-defrost refrigerator
manufactured by Whirlpool.
Prototype Unit A 90 V inverter was added to the power supply to the compressor.  The
               fan voltage and frequency was not changed.

                                 Table III.2 Inverter
— 	 . 	 _ 	 _ 	 . — . — . 	 ,— : 	 1
: Baseline Inverter
FF/FZ Temperature (°F)
Energy Consumption (kWh/24h)
Duty Cycle
% Energy Reduction
42.3/4.4
2.49
0.57

42.3/4.8
2.36
0.69
5
Discussion     The best result with the inverter was achieved at an inverter frequency
                of 45 Hz.  The test results demonstrate that there may exist an optimum
                duty cycle, which is not 100 percent, when an inverter is used.  In
                addition to using the inverter, the supply voltage was optimized and
                found to be 90V.
 34

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                                                                  Prototype Test Results
                                                                           May 1994
III.A.3.  Voltage Regulator
  i
III.A.3.O. Green Plug—New Top-Freezer Refrigerator

The "Green Plug" is a commercially available voltage regulator.  '
  t
Baselinfe Unit  The baseline unit was a 20 ft3 top-freezer automatic-defrost R/F
  !             manufactured by Whirlpool in 1992, model number ET20ZKXZW.

Prototype Unit Baseline R/F was connected to a 115V and 120V power supply via the
  !             Green Plug.
  t                                .
  ;               Table III.3 Green Plug—New Top-Freezer Refrigerator
i Green
; Baseline Plug
Input Voltage (V)
Energy Consumption (kWh/24h)
FF/FZ Temperature (°F)
Duty Cycle
% Energy Reduction
115
2.47
37.1/4.0
0.54

115
2.37
35.2/4.9
0.54
4
; . • '• . - ' - - *
i - ; V "
i Green
i Baseline Plug
i . o
Input Voltage (V)
Energy Consumption (kWh/24h)
FF/FZ Temperature (°F)
Duty Cycle
% Energy Reduction
120
2.41
38.2/8.4
0.48

120 ,
2.40
38.7/8.6
0.45
0
Discussion     Generally, test results with this refrigerator showed performance
  i             changes of about 2+3 percent when the Green Plug was used.  Similar
               results have been found by Consumers Union. [10]
                                                                                35

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Energy-Efficient Refrigerators
IILA.3.b Green Plug—Side-by-Side Refrigerator

The Green Plug is a commercially available voltage regulator.

Baseline Unit  The baseline unit was a 1975 Sears 19 ft3 side-by-side R/F, model
               number 106-7650511.

Prototype Unit The baseline unit was connected to a 115V and 120V power supply via
               the Green Plug.

                   Table ILIA Green Plug—Side-by-Side Refrigerator
... ' v i : •! * .'(•••-.••.
'.' : ' : ,| • I i Green ;
: ' ; ; 1 Baseline r Plug
Input Voltage (V)
Energy Consumption (kWh/24h)
FF/FZ Temperature (°F)
Duty Cycle
% Energy Reduction
120
5.34
34.1/8.2
0.67

120
5.35
34.4/8.4
0.69
0
! -.{ '. ! ! - l
: : - | ; ' Green;
j -j 'j ' Baseline Plug
Input Voltage (V)
Energy Consumption (kWh/24h)
FF/FZ Temperature (°F)
Duty Cycle
% Energy Reduction
120
6.11
30.1/3.8
0.75

120
5.75
30.9/4.2
0.68
6
Discussion     Generally, test results with this refrigerator showed performance
               changes of about minus two to six percent when the Green Plug was
               used.  Only at 120V and under severe operating conditions (high
               temperature lift) were savings of 6 percent found.  These results are also
               consistent with results found by Consumers Union. [10]
36

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                                                                 .Prototype Test Results
                                                                      	May 1994
III.A.4 Hot Water Refrigerator
Baseline Unit
The baseline R/F was an 18 ft3 top-freezer automatic-defrost unit
produced by Whirlpool, model number ET18ZKXZWOO.
Prototype Unit A water-cooled condenser was added before and in series with the
               condenser of the baseline R/F. The water loop for the water-cooled
  i             condenser was equipped with a 5-gallon water tank and a circulation
  I             pump. Whenever the refrigerator was in operation, the pump operated
  !             and the condenser fan was turned off. If the water temperature in the
  I             tank rose above the set point, the pump would turn off, and the
  t             condenser fan would come on. The water-cooled condenser was a tube-
  j             in-tube, counter-flow heat exchanger with refrigerant in the inside tube.
  j             Outside and inside tubes were 0.375"  and 0.125" in diameter, and the
  I             condenser was about 120" long.

                         Table III.5 Hot Water Refrigerator
i Baseline Prototype
Energy Consumption (kWh/24h)
FF/FZ Temperature (°F)
Water Flow Rate (g/s)
Initial Temperature in Water Tank (°F)
Final Temperature in Water Tank (°F)
Heat Recovered to Water Tank
(kWh/24h)
Duty Cycle
1.86
38.9/3.5
n/a
n/a
n/a
n/a
0.46
2.09
36.0/4.1
14.5
: 72
118
1.26
0.33
Discussion     While the energy consumption of the prototype R/F was higher than for
  ;             the baseline, the heat recovered by the water-cooled condenser reduced
  j             the energy requirement of the water heater.  Results of a simulation of a
               domestic water heater combined with the measured refrigerator
               performance show net energy savings of 10 to 15 percent for the
  !             combined system.
                                                                                37

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Energy-Efficient Refrigerators
III.B.   IMPROVED REFRIGERANTS

III.B.1  Improved Refrigerants—Hydrocarbon Blends
Baseline Unit
The baseline unit was a 20 ft3 top-freezer automatic-defrost R/F
produced by Whirlpool, model number ET20ZKXZW.
Prototype Unit A mixture of n-butane (R-600) and propane (R-290) was used as a
               refrigerant in the original refrigerator.  The capillary tube length and
               charge were optimized.  A sight glass at the condenser outlet and two
               pressure transducers were also added. The additional capillary tube had
               a diameter of 0.026".

                           Table III.6 Hydrocarbon Blends
Baseline R-600 and R-290
1 ' i i . " i - -i
Charge (g)
Extra Cap. Tube (ft)
Energy Consumption (kWh/24h)
FF/FZ Temperature (F)
Duty Cycle
% Energy Reduction
240
0
2.47
37.1/4.0
0.54

80 (30/70)
5
2.30
39.4/3.3
0.33
7
Discussion     There are a number of advantages that result from hydrocarbon use:
               energy savings up to seven percent compared to R-12 as the refrigerant,
               charge reduction to a third of that of R-12, and a lower pressure ratio
               than that of R-12.  The energy savings can be improved by taking
               advantage of the temperature glide (which was not done here). The
               charge can also be reduced further with better designs, thereby reducing
               the flammability risk.  It should be noted that the mixture concentration
               may vary considerably due to preferential oil solubility and storage
               effects in components. [11]
38

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                                                                  Prototype Test Results
                                                                           May 1994
III.B.2  Improved Refrigerants—Cyclopropane
Baseline Unit  The baseline R/F was an 18.0 ft3 top-freezer automatic-defrost unit
  i             manufactured by Whirlpool.

Prototype Unit Only the refrigerant, amount of charge, and the length of the capillary
  i             tube were changed.

  j                            Table IIL7 Cyclopropane
Baseline Cyclopropane
Charge (g)
Energy Consumption (kWh/24h)
FF/FZ Temperature (°F)
Duty Cycle
% Energy Reduction
156
2.20
38.5/4.4
0.52

100
2.05
38.9/4.4
0.47
7
Discussion     Cyclopropane showed a seven percent decrease iri energy consumption
               compared to the baseline with R-12.  The volummetric capacity of
               cyclopropane is 17 percent higher than that of R-12. Since the
  j             compressor remained unchanged, the higher volummetric capacity
  i             resulted in a reduction of the compressor run time.  The discharge
               pressure of cyclopropane increased by 10 percent, while the suction
  ,             pressure was similar to that of R-12.  [12]

  !             ERA predicted a four percent energy reduction when HFC-134a was
               replaced by cyclopropane. [2]
                                                                                 39

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Energy-Efficient Refrigerators
III.B.3 Improved Refrigerants—HFC-134a and HFC-152a

Original Unit  The original unit was an 18.0 ft3 top-mounted automatic-defrost R/F
               built by GE, model number TBX18P.

Prototype Unit The original compressor was replaced with a RG108-1 compressor for
               HFC-134a tests.  It was then replaced with a TG108-1 compressor for
               HFC-152a tests.  Both compressors came from AMERICOLD. •

         Table HL8  Minimum Energy  Consumption of the Optimized Systems
System bfype . '. \ HFC-134a HFC-152a
Min. energy consumption (kWh/day)
Avg. instantaneous power (on time) (W)
Compressor on-time (min)
Total cycle time (min)
Additional capillary tube length (ft)
Refrigerant charge (g)
Avg. freezer comp. temperature (°F)
Avg. food comp. temperature (°F)
Avg. evap. pressure during on time (psia)
Avg. cond. pressure during on time (psia)
1.83
172.4
23.0
52.0
7.0
200
5.6
40.8
15.1
174.0
1.79
174.0
21.0
49.0
18.0
120.
5.1
40.3
13.3
163.3
                Table III.9 Calorimeter Data for the Two Compressors
' ;- .:•!;. I . . ' ! '• : :.
Refrigerant i HFC-134a HFC-152a
' : ' [ ! i
Compressor model #
Oil type
Evaporation teinperature (°F)
Evaporation pressure (psia)
Condensing temperature (°F)
Condensing pressure (psia)
Capacity (BTU/h)
EER
RG108-1
RL212B (Ester)
-10.4
16.5
129.9
213.4
759.9
4.78
TG108-1
100DL (alkylbenzene)
-9.4
15.4
129.8
190.3
824.7
4.93
Discussion     The HFC-152a R/F test has two percent lower energy consumption than
               the HFC-134a R/F test. The calorimeter tests show a three percent lower
               EER and an eight percent lower capacity for the HFC-134a compressor.
               The lower capacity of the compressor is reflected in the longer run time
               for the HFC-134a R/F.  When the lower EER of the HFC-134a
               compressor is considered, both systems have the same performance. [13]
40

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                                                                  Prototype Test Results
                                                                           Mai/1994
III.B.4 Improved Refrigerants—HCFC-22 and HFC-152a Blends
Baseline Unit  The baseline R/F was a GE 18 ft3 top-freezer automatic-defrost unit.
  i
Prototype Unit There were essentially no changes made to the refrigerator, except
  i             changes to the capillary and the addition of measurement probes (two
               pressure transducers and one sight-glass).

                     Table 111.10 HCFC-22 and HFC-152a Blends
' 1 ' :
i Babeline 13% HCFC-22 and 87% HFC-152a
Charge (g)
Energy Consumption (kWh/24h)
FF/FZ Temperature (°F)
1
I
Duty Cycle
% Energy Reduction
350
2.11
44.3/5.0
0.48

207 (27&180)
2.03
43.7/4.8
0.48
4
Discussion     Several mixture compositions were tried to find the mixture of 13
               percent HCFC-22 and 87 percent HFC-152a.  This best mixture led to an
               optimum energy savings of four percent. [12]
                                                                                41

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   Energy-Efficient Refrigerators
m.C. IMPROVED CYCLE

IH.C.l  Lorenz-Meutzner Cycle

IILC.l.a Lorenz-Meutzner Cycle—Zeotropic Refrigerant Mixtures

Baseline Unit   The baseline R/F was a 20.0 ft3 side-by-side unit produced by Whirlpool.

Prototype Unit  The original evaporator was replaced by a counter-cross-flow evaporator, and
                a natural convection evaporator was added to the fresh food compartment.
                The total internal volume of the two evaporators was 72 percent of the original
                evaporator volume, resulting in a reduction of the charge. The original 10W
                freezer evaporator fan was replaced with a 7W unit,  and a small 1W DC fan
                was placed in the fresh food cabinet to eliminate temperature gradients.  A
                combination of two counter-current tube-to-tube heat exchangers (high and
                low temperature) and an adiabatic capillary tube replaced the conventional
                suction line heat exchanger.  The original reciprocating compressor and
                condenser were used. The original compressor oil, a 150 SSU mineral oil
                (naphthenic), was used for tests involving R-12.  A synthetic oil (alkylbenzene)
                was used with the zeotropic refrigerant mixture. A commercial filter dryer
                was installed in the liquid line after the condenser.  Additional details on the
                various components can be found in reference [14].

             Table III.ll Lorenz-Meutzner Cycle—Zeotropic Refrigerant Mixtures
                          Baseline
                          ' (R-12)
:. 65% HCFC-22 •-
     and
35%HCFC-123
 71% HqFC-22
     and
29% HCFC-141b
60% HCFC-22
    and
40% HCI-C-123
Energy Consumption
(kWh/24h)
FF/FZ Temperature (°F)
Duty Cycle
% Energy Reduction
2.44
36.6/4.5
0.57

2.17
36.2/5.0
0.53
11
2.20
40.0/4.9
0.51
10
2.26
38.0/4.9
0.58
7
Discussion     This prototype demonstrates that the Lorenz-Meutzner cycle works well in a
                side-by-side refrigerator/freezer.  The natural-convection food-compartment
                evaporator caused significant temperature stratification that could be
                eliminated with a 1W fan.  Consequently, a forced-convection evaporator is
                recommended for the food compartment in a side-by-side unit.
   42

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                                                                          Prototype Test Results
                                                                                   May 1994
      IILC.l.b Lorenz-Meutzner Cycle—Hydrocarbon Blends

      Baseline Unit   The baseline unit was an 18.0 ft3 top-freezer automatic-defrost R/F built
         :             by Whirlpool, model number WT18NKYO.

      Prototype Unit A natural convection food compartment evaporator, a counter-flow
         |             freezer evaporator, and a suction line heat exchanger were added to the
         1             baseline R/F.
         1

                     Table IIL12 Lorenz-Meutzner Cycle—Hydrocarbon Blends


Baseline Baseline
Cycle Baseline LM 1 ,LM 2 L-M L-M L-M L-M
! i
; '
Refrigerant
Charge (g)
Energy Consumption
(kWh/24h)
f
FF/FZ T

emperature

% F^nergy Reduction
Test Date


R-12
300
1.83
38.1 /
4.7


10/91
original
R-12
310
1.69
38.5/
5.0

8
* 09/92

R-12
360
1.84
38.1/
4.7

-1
* 05/93

R-290/
C5H12
180
(50/50)
1.54
40.4/
4.8

16


R-290/
HCFC-123
180
(50/50)
1
1.52
38.9/
4.7

17
:

R-290/
R-600
145
(48/52)
1.52
38.8/
5.1

17


R-290/
R-600/
157
(42/S9/
19)
1.50
40.2/5.1

18


* After conversion to Lorenz-Meutzner cycle


      Discussion     Hydrocarbon mixtures in the Lorenz cycle save energy in the range from
         I             16 to 18 percent as compared to R-12 in a top-freezer automatic-defrost
         I             refrigerator. If it is considered that the refrigerator insulation tends to
         !             age over time  (increasing of thermal conductivity), which may be
         t             indicated by the difference in the baseline tests LM1 and LM2 with
         j             otherwise identical hardware, then the savings will reach 23 to 25
         I             percent.
                                                                                        43

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Energy-Efficient Refrigerators
                ERA predicted 18 percent energy reductions for similar R/Fs with
                natural convection evaporators in the fresh food compartment.  This is
                in agreement with the test results.
44

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                                                                    Prototype Test Results
                                                                             May 1994
III.C.l.c  Lorenz-Meutzner Cycle

Baseline Unit   The baseline R/F was a 19.8 ft3 top-freezer automatic-defrost unit
   I             produced by Whirlpool, model number ET20ZKXZW.
   i
Prototype Unit A counter-cross-flow condenser (forced convection), counter-flow freezer
   |             evaporator (forced convection), counter-flow food compartment
   I             evaporator (natural convection) were added. An inter-cooler between
   1             the freezer and fresh food evaporators was not used.

   1                       Table IIL13 Lorenz-Meutzner Cycle
I 1
Heater On Off Off Off On On
Refrigerant
FF/FZ Temperature
(PF)
Energy
Consumption
(kWh/24h)
% Energy
Reduction**
R-12
41.9/5
2.17

R-12
38.6/5
2.05

Mixture 1*
38.5/4.5
1.74
15
Mixture 2*
42.0/5.2
1.66
19
R-12
41.8/4.8
!- 2.28

Mixture 2*
42.3/4.8
1.92
16
   Mixture 1 is HFC-134a (56%)/HCFC-123 (31%)/R-290 (4%)/HFC-32 (9%), and (Mixture) 2 is R-290
   (65 %)/HCFC-123 (35%). • •                   -                      ;
   i                                                            |
  Compared •with the test result using R-12.
Discussion     The R-12 test was repeated (second to last column) to account for the
   !             aging of the cabinet and any other deterioration of the insulation that
                may have occurred during the numerous modifications.  The energy
   1             savings are calculated based on the respective baseline test (either with
   I             the heater on or off). The savings of the last test are based on the latest
   :             baseline.  Test results show that at least 15 percent energy savings can
   i             be achieved with this version of the Lorenz-Meutzner cycle.
                                                                                   45

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Energy-Efficient Refrigerators
III.C.2  Modified Lorenz-Meutzner Cycle

III.C.2.a Modified Lorenz-Meutzner Cycle—U.S. Refrigerator

The modified Lorenz-Meutzner cycle has three-way internal heat exchangers in the food
and freezer compartments, where heat is mutually exchanged between the compartment
air, refrigerant condensate, and evaporating refrigerant. In the original Lorenz-Meutzner
Cycle, heat is internally exchanged between the compartment air and refrigerant vapor,
while the refrigerant condensate line is bypassed.
Baseline Unit
The baseline R/F was a 19.8 ft3 top-freezer automatic-defrost Whirlpool
(Kitchen Aid) unit, model number KTRS20KXWH10.
Prototype Unit A modified Lorenz-Meutzner cycle with internal heat exchange in the
               evaporators, counter-cross-flow condenser and freezer evaporator,
               natural-convection food evaporator, and intercooler added.  The
               refrigerator/freezer was equipped with the original rotary compressor
               and energy-saving valve.

            Table IIL14 Modified Lorenz-Meutzner Cycle—IT.S. Refrigerator
''.'•: : ;; Baseline - i Prototype
Refrigerant
Energy Consumption (kWh/24h)
FF/FZ Temperature (°F)
% Energy Reduction
R-12
1.86
38.1/5.1

R-290/HCFC-123
1.55
38.6/4.1
17
Discussion     The results indicate that the daily energy consumption decreased by up
               to 17 percent without considering the defrost cycle. Many other CFC-free
               refrigerant mixtures were also tested with significant energy savings, in
               the same 17 percent savings range.
46

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                                                                   Prototype Test Results
                                                                            May 1994
III.C.2.b Modified Lorenz-Meutzner Cycle—Chinese Refrigerator
Baseline Unit
The baseline R/F was a top-freezer 6.4 ft3 automatic-defrost model
produced by the ShangLing Refrigerator Co., model number BCD-180.
Prototype Unit  Modification similar to those described in Section IH.C.2.a were made.
                The evaporator was constructed of 5/16 inch O.D. aluminum/copper
  !              tubing in a cross-counter-flow pattern with 40-45 plate fins.  The
  !              resulting heat exchanger was 9 inches deep in the direction of air flow
  I              with 12.5 inch x 2 inch cross-sectional area.
  f
  :        Table 111.15 Modified Lorenz-Meutzner Cycle—Chinese Refrigerator
   Refrigerant
                                            Baseline
                              R-12
                                                   Prototype
  R-290/
HCFC-123
   Energy Consumption (kWh/24h)
                               1.29
   1.16
   FF/FZ Temperature (°F)
                             38.7/5.0
 38.1/5.0
  ' % Energy Reduction
                                                      10
Discussion     The results indicate that the daily energy consumption decreased by up
  ,             to 10 percent. Since this Chinese refrigerator had much smaller internal
  j             volume, there was not much room for optimizing the evaporators. Also,
  I             the condenser was located in the foam insulation and was not a counter-
               flow design.  Considering these limitations, the energy savings were
               quite good, although not as high as found in the American R/F.  [15]
                                                                                 47

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Energy-Efficient Refrigerators
III.C.3 Dual-Loop System
Baseline Unit
Prototype Unit
The baseline R/F was a 19.8 ft3 top-freezer automatic-defrost unit
manufactured by Whirlpool.

A dual-loop system with two separate vapor compression cycles, one
for the freezer and one for the food compartment, were added. The
freezer compartment cycle included a 4.0 EER reciprocating
compressor, which was placed at the left outside of the cabinet, the
original evaporator and fan, mounted in the original position, and a
natural convection condenser located on the back of tine cabinet.

The food compartment cycle consisted of a 3.65 EER reciprocating
compressor, located in the original compressor compartment, a new
counter-flow heat exchanger with a 6 W fan, and a new natural
convection condenser.

To reduce heat transfer between the two compartments, the top side
of the food and the bottom side of the freezer compartments were
insulated with a 1-inch thick glass wool mat. The compressor oil was
changed from a mineral oil with 3GS viscosity  to a 1GS mineral oil to
compensate for  the lower operating temperatures.  Additional details
can be found in reference [16].

         Table 111.16 Dual Loop System
I ! Baseline ' DuallLoop
Energy Consumption (kWh/24h)
FF/FZ Temperature (°F)
Duty Cycle
% Energy Reduction
1.98
40.5/3.7
0.47

1.87
(1.3.0 in FF + 0.57 in FZ)
39.6/3.7
0.51 for FZ/0.22 for FF
4
Discussion     The best result achieved with the dual loop system showed a four
               percent improvement of the total energy consumption over the baseline.
               The compressors used in both cycles were smaller and lower EER than
               the original rotary compressor (EER = 4.9). Energy savings of more than
               20 percent could be possible, if compressors with the same EER as the
               original compressor were available. The reported savings exclude
               defrost.  Higher energy savings can be expected when defrost is
               included.  This effort continued for an additional 12 months with the
48

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                                                   Prototype Test Results
                                                            May 1994
best result being a 4 percent reduction in energy consumption.
Accounting for foam aging, the result would have been higher.

ERA calculations for the dual loop have predicted a two percent energy
reduction.  The savings were smaller because forced convection
evaporators and condensers  were used. [2]
                                                                  49

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Energy-Efficient Refrigerators
III.C.4  Two-Stage Refrigerator
Baseline Unit
The baseline model was built at U. Md.  It consisted of an approximately
20 ft3 top-freezer refrigerator that was housed in an insulated wooden
box.
Prototype Unit  A forced convection food compartment evaporator, forced convection
                freezer evaporator, and condenser were used.  Two compressors were
                used in series. The first pumped refrigerant from the freezer evaporator
                to the food compartment evaporator pressure level, the second from the
                fresh food pressure level to the condenser pressure level.

                            Table 111.17 Two-Stage System
•i^MMl
Energy Consumption (kWh/24h)
FF/FZ Temperature (°F)
Duty Cycle
FF/FZ Compressor EER
Charge (g)
% Energy Reduction
r - "
Baseline j pfwo-Stage
3.30
43.9/5.2
0.72
4.4
480

3.20
38.3/5.3
0.62
4.2/3.4
316
3
Discussion     The test results show a three percent energy savings over the single
               stage configuration.  Considering that the food compartment
               temperature was considerably lower than in the baseline test, another
               three percent could have been gained. Finally, accounting for the lower
               compressor EER would result in a total energy savings of about 20
               percent.
50

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                                                                  Prototype Test Results
                                                                           May 1994
III.C.5 Kopko Cycle
The Kopko cycle represents a method of achieving energy savings with two evaporators
in 3 single circuit without the use of mixtures or special control valves. The basic set-up
uses a freezer evaporator and fresh-food evaporator connected in series, each with its
own fan.  The controls run one evaporator fan at a time.  Only the freezer fan operates
when cooling the freezer; and only the fresh-food compartment fan operates when
cooling the fresh-food compartment.  The evaporators are installed to minimize natural
convection of air when the fans are off. The normal sequence is to cool the fresh-food
compartment first, then the freezer.  This set-up uses the higher evaporator pressures
that normally occur at the beginning of the compressor on time to cool the fresh-food
compartment.
Baseline Unit
The baseline unit was an 18 ft3 top-freezer automatic-defrost R/F
manufactured by Whirlpool, model number ET18NKXYW.
Prototype Unit A forced convection food compartment evaporator was added to the
   •            system. Capillary tube length was optimized and measurement probes
   j            were added.  The control logic was changed. Lastly, the compressor
   I            was exchanged as indicated in the table below. [17]

   ;                           Table 111.18 Kopko Cycle
Baseline Kopko
i
Energy Consumption (kWh/24h)
FF/FZ Temperature (°F)
Duty Cycle
Compressor
HER
Charge (g)
% Energy Reduction
1.78
38.4/4.9
0.45
FGV80AW(SINGLE)
4.91
177

1.24
39.0/5.1
0.43
AMERICOLD HG107
5.52
360
30
Discussion     The use of the Kopko configuration leads to considerable energy
   i            savings.  When the higher compressor EER is excluded, the new
               configuration produces an 18 percent increase in performance.

   ,            The following six tables describe all of the intermediate modifications to
   i            the Kopko system and the respective  test results.
                                                                                51

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Energy-Efficient Refrigerators
                      Table IIL19 Kopko Cycle—First Modification
' Baseline First Modification '-.
> 1 i i i . 1
Size
Compressor
Freezer Evaporator
Type
Total Area
Flow
Fan
Food Evaporator
Type
Total Area
Flow
Fan
Condenser
Capillary Tube
SLHX
Fan Control
R-12 Flow Path Direction
R-12 Charge (g)
Two-Way Switch
Model #
Power
On-time Delay Relay
Model #
Power
Filter Dryer
Sight-glass
18ft3
FGV80AW
Forced Convection
Plate Fin and Tube
2,500 in2
Cross-Flow
40 - 50 cfm, 8 - 12 W
N/A
Natural Convection
~8' (0.026" ID)
6'8"
0.026" ID by 0.313" OD
N/A
N/A
177
N/A
N/A
Original
N/A
Same as Baseline
Same as Baseline
Forced Convection
Spiny Fin and Tube
1,457 in2(0.94 m2)
Counter-Flow
Same as Baseline
Forced Convection
Plate Fin and Tube
2,500m2
Cross-Flow
65cfm, 7W
Pewee Boxer
Model* 4715PS-12T-B10
Same as Baseline
9'6" (0.026" ID) in FZ
10' (4' located in FF)
0.125" by 0.313"OD
FZ Fan First with Timer ,
FZ to FF Evaporator
230
Potter-Brumfield
KUP-5A15-120
2W
Dayton Elect. MFG. Co.
6X601F (Range 9-900sec)
3 W
ALCO
EK - 032
Installed
52

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                                                                  Prototype Test Results
                                                                           May 1994
            Table 111.20 Kopko Cycle—First Modification Test Results
Energy Consumption
,(kWh/24h)
                                      Baseline
  1.78
                        First Modification
   1.67
^Z/FF Temperature (°F)
4.9/38.4
 4.7/38.2
kTD Controller
Set Point, FZ/FF (°F)
jHysterisis, FZ/FF
  5.5/-
  1.4/-
4.5/38.55
 0.4/0.3
Puty Cycle
  0.45
  0.42
% Energy Reduction
                                                                                53

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Energy-Efficient Refrigerators
                     Table 111.21 Kopko Cycle—Second Modification
First Modification Second Modification :
Compressor
Freezer Evaporator
Type
Total Area
Flow
Fan
Food Evaporator
Type
Total Area
Flow
Fan
Condenser
Capillary Tube
SLHX
Fan Control
R12 Flow Path
Direction
R12 Charge (g)
Two-Way Switch
On-time Delay Relay
Filter Dryer
Sight-glass
Special Insulation
Mullion
FZ Evaporator Cover
FGV80AW
Forced Convection
Spiny Fin and Tube
1,457 in2
Counter-Flow
40 - 50 cfm, 8 - 12 W
Forced Convection
Plate Fin and Tube
2,500 in2
Cross-Flow
65 cfm, 7 W
Pewee Boxer
Model* 4715PS-12T-B10
Natural Convection
9'6" (0.026" ID) in FZ
10' (4' located in FF)
0.125" by 0.313"OD
FZ Fan First with Timer
FZ to FF Evaporator
230
Installed
Installed
Installed
Installed
N/A
FGV80AW .'
Forced Convection
Spiny Fin and Tube
2,853 in2 (1.84 m2)
Counter-Flow
26 cfm, 4 W
Forced Convection
Plate Fin and Tube
3,661 in2 (2.36 m2)
Cross-Flow
65 cfm, 7 W
Pewee Boxer
Model* 4715PS-12T-B10
Natural Convection
8'0" (0.026" ID) in FZ
6'8"
0.026'TD by 0.313"OD
FF Fan First
FZ to FF Evaporator
300
Installed
N/A
Installed
Installed
1" Foam
Glass Wool
54

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                                                         Prototype Test Results
                                                         	   "May~1994
Table 111.22 Kopko Cycle—Second Modification Test Results
: " =: 1-
Eirst Second
; i ,
Modification . Modification
Energy Consumption (kWh/d)
FZ/FF Temperature (°F)
RTD Controller
Set Point, FZ/FF (°F)
Hysterisis, FZ/FF ;
Pressure (psia)
High Side-
Low Side
Temperature (°F)
Condenser
FZ Evaporator
FF Evaporator
On/Off-Time (min)
FF On-Time (min)
Duty Cycle
% Energy Reduction from
Baseline
1.67
4.7/38.2
4.5/38.55
0.4/0.3 .
161.6
15.5
105.2
-21.3
9.5
12.8/18.0
- (Fan on once)
0.42
6
1.56
5.0/38.3
5.9/36.9
1.0/0.2
158.1
16.2
113.0
-15.8
-3.9
13.5/19.7
4.5 (Fan on twice)
0.41
1
12
                                                                         55

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Energy-Efficient Refrigerators
             Table 111.23 Kopko Cycle—Third Modification and Test Results
: • - : • ' 1 . .' ' 1 • ' ' •
• Second Modification Third Modification
Energy Consumption
(kWh/d)
FZ/FF Temperature
RTD Controller
Set Point, FZ/FF (°F)
Hysterisis, FZ/FF
Pressure (psia)
HigltySide
Low Side
Temperature (°F)
Condenser
FZ Evaporator
FF Evaporator
Compressor
Model*
Capacity
EER
Oil

R12 Charge (g)
On/Off-Time (min)
FF On-Time (min)
Duty Ctcle
% Energy Reduction
from Baseline
1.56
5.0/38.3

5.9/36.9
1.0/0.2
158.1
16.2
113.0
-15.8
-3.9
Reciprocating
FGV80AW
(EMBRACO)
820
4.91
Mineral, 3GS
300
13.5/19.7
4.5
0.41
12
1.29
5.1/ 39.2 .

5.35/36.25
0.7/0.7
152.2
15.5
97.5
-17.5
12.3
Reciprocating
HG-107
(AMERICOLD)
700
5.5
Mineral, 1GS
320
13.3/16.3
5.5 ,
45
28
56

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                                                          Prototype Test Results
                                                            	May1994
Table 111.24 Kopko Cycle—Fourth Modification and Test Results
I 1
Third Modification Fourth Modification
; -
Energy Consumption
(kWh/24h)
FZ/FF Temperature
! (°F)
! RTD Controller
| Set Point, FZ/FD (°F)
! Hysterisis, FZ/FD
Pressure (psia)
High /Low Side
Temperature (°F)
Condenser
FZ/FF Evaporator
Compressor
1 Model*
[ Capacity
EER
Oil
: R12 Charge (g)
Filter Dryer
Sight-glass
On/Off-Time (min)
FF On-Time (min)
Duty Cycle
% Energy Reduction
from Baseline
1.29
5.1/39.2
5.35/36.25
0.7/0.7
152.2/15.5
97.5
-17.5/12.3
Reciprocating
HG-107 (AMERICOLD)
700
5.5
Mineral, 1GS
320
Installed
Installed
13.3/16.3
5.5
0.45
28
1.24
5.1/39.0
4.0/35.2
1.5/0.6
150.1/16.2
95.0
-15.2/42.8
Reciprocating
HG-107 (AMERICOLD)
700
5.5
Mineral, 1GS
320
Removed
Removed
20.8/28.0
7
0.43
30
                                                                          57

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Energy-Efficient Refrigerators
58

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                                                                Prototype Test Results
                                                                         May 1994
IV.  SYSTEM AND CABINET MODIFICATIONS
Several super-efficient prototype units have been built and tested combining
modifications to both the system and cabinet.  These units are described in this section.
                                                                              59

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Energy-Efficient Refrigerators
IV.A DOUBLE INSULATION AND LORENZ-MEUTZNER CYCLE
Baseline Unit  The baseline model was a 20 ft3 top-freezer automatic-defrost R/F
               produced by Whirlpool. This was the same unit described in
               Section II.A.1.

Prototype Unit A series of modifications were made to the prototype unit. These
               included adding double insulation (see II.A.1), adding a high-efficiency
               compressor, adding a modified Lorenz-Meutzner cycle with a HCFC-123
               and R-290 refrigerant blend, and reducing the gasket region heat leak.
               The results of each step in the path follow.  Details of individual steps
               are then presented. [18]

                Table W.l Double-Insulated, Lorenz-Cycle Refrigerator
In$ulatlon Standard Double Double Double Double DOUBLE
Compressor*
Cycle
Door Seal
Refrigerant
Charge (g)
FF/FZ Temp. (°F)
Duty Cycle
Energy Consump.
(kWh/24h)
Energy Consump.
including defrost
% Energy
Reduction
Total % Energy
Reduction
Standard
Standard
Standard
R-12

38/5

1.86



Standard
Standard
Standard
R-12
220
37.0/5.3
0.36
1.36
1.47
27
27
High Eff.
Standard
Standard
R-12
220
37.2/5.4
0.39
1.26
1.38
7
32
High Eff.
Lorenz
Standard
R-12
410
36.4/5.9
0.39
1.25
N/A
1
33
High Eff.
Lorenz
Standard
HCFC-123
and R-290
210
38.6/5.4
0.26
1.05
1.20
16
44
High Eff.
Lorenz
Improved
HCFC-123 and
R-290
210
38.5/5.5
0.25
1.01
1.14
4
46
*Sce Table IV.2. for additional information.
Discussion     The next four sections provide design details
                Detailed comparison of the test results and a
                improved door seal are also attached.
of the prototypes tested.
drawing showing the
60

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                                                                   Prototype Test Results
                                                                            May 1994
IV.A.1  Double Insulation
These modifications are described in Section II.A.I.
IV.A.2  High-Efficiency Compressor
The calorimeter test data for the high-efficiency compressor were provided by the
manufacturer.  Table IV.2 compares the original rotary compressor with the high
efficiency reciprocating compressor.  The EER of the new compressor was about 12
percent higher than that of the conventional compressor used in the original thick wall
unit. [18]

    ,                    Table IV.2 High-Efficiency Compressor
' \
Original High Efficiency
Compressor Compressor
Model
Type
Oil
Oil Viscosity
EER (BTU/W-h)
Capacity (BTU/h)
Power (W)
RA53L11RA
Rotary
Alkylbenzene
3GS
4.80-4.86
850-867
177
HG107
Reciprocating
Mineral Oil
1GS
5.50-5.54 ,
703.2-713.4
129
                                                                                  61

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Energy-Efficient Refrigerators
IV.A.3 Modified Lorenz-Meutzner Cycle
A modified Lorenz-Meutzner cycle was incorporated into the R/F.  See section III.C.l.c
for additional details. Table IV.3 compares the specifications of the standard and new
cycles.

                     Table IV.3 ModifiedTLorenz-Meutzner Cycle
                       Double Insulated with
                          High Efficiency
                            Compressor
    Modified
Lorenz-Meutzner
     Cycle
Size
Compressor
Compressor Oil
Freezer
evaporator
Cabinet
evaporator
Condenser
Suction line HX
Low temp. HX
19.9 cubic feet
HG107
Alkylbenzene
Forced convection tube and fin,
18 tube passes, 26" each pass,
3/8" OD, 77 fins, cross-flow
type
None
Forced convection
0.026" ID capillary tube
soldered to 5/16" OD suction
line
None
Less than 19.9 cubic feet
(considering space of cabinet
evaporator)
HG107
Mineral oil
Forced convection tube and fin,
18 tube passes, 25". each pass,
3/8" OD counter-cross flow
Natural convection copper flat-
plate, 28" by 26", copper plate
two side with thickness 1/32",
total surface area 1456 in2
Forced convection, modified to
counter flow
1/8" OD soldered to 5/16" OD
suction tube, same length as the
original length
25" long 3/8" OD and 1/8" OD
tube soldered together, two
passes
 62

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                                                          ; ,  Prototype Test Results
                                                          :     	May 1994
IV.A.4  Improved Gasket
    t
The cabinet flange was modified to reduce heat leakage into the cab:inet as described in
Section II.C.l. A drawing of the modified gasket region follows.
              Figure IV.l Schematic Representation of Improved Gasket
                  insulation tape
                  2 inches in width
                  1/8 inch in thickness
                              Freezer Compartment
                            Fresh Food Compartment
                                Front View
                                                                           63

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Energy-Efficient Refrigerators
IV.B DOUBLE INSULATION AND KOPKO CYCLE
Baseline Unit  The baseline model was the 20 ft3 R/F described in Section II.A.1.

Prototype Unit Double insulation (section II.A.I) and the Kopko cycle (Sectidn III.C.5)
               were added to the baseline model.

                Table IV.4 Double-Insulated, Kopko-Cycle Refrigerator
\ : :
; Baseline Double Insulation ; Kopko
Energy
Consumption
(kWh/24h)
FF/FZ
Temperature (°F)
Duty Cycle
Compressor
EER
% Energy
Savings
Total % Energy
Savings
1.86
38.1/5.1
0.45
RA53L11RA(SINGLE)
4.9


1.43
38.7/5.2
0.34
RA53L11RA(SINGLE)
4.9
23 ...
23
1.29
38.2/5.0
0.34
FN45R80T
4.5
10
31
Discussion     Accounting for the change in the compressor EER, the total energy
               savings based on the Kopko concept amounts to 19 percent. This would
               result in nearly a 40 percent reduction for the total modification. The
               following four tables describe all of the intermediate modifications to the
               system and the respective test results.
64

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                                                      Prototype Test Results
                                                                May 1994
Table IV.5 Specifications for the First Modification
Baseline First Modification
Size
Wall Insulation
Compressor
Model*
Capacity
EER
Oil
Freezer Evaporator
Type
Total Area
Flow
Fan
Food Evaporator
Type
Total Area
Flow
Fan
Condenser
; Capillary Tube
SLHX
Fan Control
I R-12 Flow Path
; Direction
R-12 Charge
Two- Way Switch
Model #
Power
Filter Dryer
Sight-glass
20ft3
Thick wall
Rotary
RA53L11RA
870.7 BTU/h(255.2 W)
4.91
Mineral, 4GS
Forced convection
Plate fin and tube
3,661in2
Cross-flow
40 - 50 cfm, 6 - 10 W
N/A
Forced convection
~ 8 ' (0.026" ID)
0.026" ID by 0.313" OD
N/A
N/A
205.5 g
N/A
Original
N/A
Same as baseline
Same as baseline
Rotary
RA48L83TE
787 Btu/h(230.7 W)
5.01
Mineral, 4GS
Forced convection
Plate fill and tube
4,265 in2(3.96 m2)
Counter-flow
65 cfm, 7W
Forced convection
Plate fin and tube
4,168 in2(3.87 m2)
Counter-flow
65 cfm, 7 W
Same as baseline
7'0" (0.026" ID) in FZ
0.125" by 0.313"OD
FF fan first
FZ to FF evaporator
410 g
Potter-Brumfield
KUP-5A15-120
2 W
Same as baseline
N/A
                                                                      65

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Energy-Efficient Refrigerators
                   Table JV.6 Test Result for the First Modification
: 1 - - j 1 • i
. , : ! • i
j Double Insulation j: First Modification
Energy Consumption
(kWh/d)
FZ/FF Temperature (°F)
Total Savings (%)
Net Saving
On/Off Time (min)
FF On-Time (min)
On-Time Ratio (%)
RTD Controller
Set Point, FZ/FF (°F)
Hysterisis, FZ/FF
1.43

5.2/38.7
-

18.1/35.5
-
33.8

5.857 -
1.27-
1.24

5.2/38.2
12.8
10.8
17.0/32.0
5.6
34.7

4.5/39.0
1.5/0.2
             Table IV.7  Compressor Comparison for Kopko Modifications
: ! : ! : 1
' •; ! ; First ; , Second
Baseline Modification Modification
Compressor
Model #

Capacity (BTU/h)
EER (%)
Oil
Rotary
Matsushita
RA53L11RA
870.7(255.2 W)
4.91
Mineral, 4GS
Rotary
Matsushita
RA48L83TE
787.0(230.7 W)
5.01 (+ 2.0)
Mineral, 4GS
Rotary
Matsushita
FN45R80T
715.0(209.5 W)
4.5 (- 8.4)
Mineral, 4GS
66

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                                                           _"-"••' Prototype Test Resutis
                                                                          Way'1994
 IV.C DOUBLE INSULATION AND ALTERNATE REFRIGERANTS
 IV.C.1 HFC-152a
Baseline Unit  The baseline model was an 8.5 ft3 bottom-freezer R/F produced by
   i            Qingdao Haier in China, model number BCD-220.  The standard cycle
   ,            includes two evaporators and a single compressor with a switching
   j            valve to control refrigerant flow.
   I
Prototype Unit Double insulation and cycle modifications were made to the unit.
   I            Added insulation was 0.8 inches on the sides, back, and bottom and 0.6
   ;            inches to the doors. Cycle improvements included, adding a counter-
   {            flow condenser (natural convection), a counter-flow freezer evaporator
   j            (three-way heat exchanger, natural convection), and a food compartment
   j            evaporator (natural convection). An inter-cooler was not added between
   s            the freezer and food compartment evaporators. A high-efficiency
   |            compressor obtained from AMERICOLD (TG105-12) was also used.

   ;           Table IV.8 Increased Insulation with Refrigerants HFC-152a
Refrigerant R-12 HFC-152a
Energy Consumption (kWh/24h)
Compressor EER
FF/FZ Temperature (°F)
% Energy Reduction
1.70
3.62
38.0/5.0

0.96
4.48
38.0/5.1
44
Discussion     The results show that the combination of modifications reduced the
               energy consumption by about 44 percent.
                                                                               67

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Energy-Efficient,Refrigerators
IV.C.2 Hydrocarbon Mixtures
Baseline Unit  The baseline unit was the same as described in the previous section.

Prototype Unit The modifications were the same as above except hydrocarbon
               refrigerants were used.

            Table IV.9 Increased Insulation with Hydrocarbon Refrigerants
  Refrigerant
  Energy Consumption (kWh/24h)
          R-290 (68i%) and    R-2^0 (63%) and
            R-600 (32%)        R-600 (37%)
  1.70
  0.80
  0.83
  FF/FZ Temperature (°F)
38.0/5.0
37.5/4.8
38.1/5.0
  % Energy Reduction
                 53
                      51
Discussion    Test results show that an additional 10 percent energy savings can be
               achieved using hydrocarbon mixtures as compared to the system using
               HFC-152a.
 68

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                                                                      Prototype Test Results
                                                                               May 1994
  V.  REFERENCES
 1.  EPA Refrigerator Analysis Program (ERA): User's Manual, Report Number EPA-430-R-93-
    007, U.S. Environmental Protection Agency, June 1993.

 2.  Multiple Pathways to Super-Efficient Refrigerators, Report Number EPA-430-R-93-008,
    U.JS. Environmental Protection Agency, June 1993.
       i
 3.  Carbon Black in Appliance Foam Insulation, }. S. Pisipati et al., in Proceedings of the 1993
    Polyurethanes World Congress, Society of the Plastics Industries, New York, October
    1993, 146-53.                                                   !

 4.  Performance Test Results for Freezers Containing Vacuum Insulation Panels, H. A. Fine and
    S. R. Griffin, Proceedings of the International Conference on Alternatives to CFCs and
    Hdlons, FGU, Berlin, Germany, 1992, 317-22.
       !                                                            I
       I                                                            I
 5.  Test Results for Refrigerator/Freezers Containing Vacuum Insulation Panels, H. A. Fine, G.
    J. Haworth and R. Srikanth, Proceedings of the International Conference on Alternatives to
    CFCs and Halons, FGU, Berlin, Germany, 1992, 305-15.
       t                                                            i

 6.  Evaluation  of Advanced Insulations for Refrigerators, G. J. Haworth, R, Srikanth, and H. A.
    Fine, Proceedings  of the 44th. Annual International Appliance Technical Conference,  Ohio
    State University,  Columbus, Ohio, May 1993, 1-12

 7.  Development and Application of Vacuum Insulation Technology to Refrigerators, G.A.
    Mellinger and K. L. Downs, presented at International Conference on CFC and Halon
    Alternatives, Washington, DC, September  1992.

 8.  Finite Element Analysis of Heat Transfer Through the Gasket Region of Refrigerator/Freezers,
    Report Number EPA-430-R-92-009, U.S. Environmental Protection Agency,
    October 1992.

 9.  Linear Compressors—A Maturing Technology, N.R. van der Walt and R. Unger, presented
    at 45th International Appliance Technical Conference, University of Wisconsin, May
    1994.

10.  "Can a Fancy Plug Cut Energy Costs?," Consumer Reports, November 1993, 694.

11.  Experimental Results with Hydrocarbon Mixtures in Domestic Refrigerator/Freezers,  B.Y. Lin,
    M4-L. Tomask and R.  Radermacher, paper sumitted to ASHRAE, April 1994.
       t
12.  R22/R152a Mixtures and Cyclopropane (RC 270) as Substitute for R12 in Single-Evaporator
    Refrigerators: Simulation and Experiments, K. Kim, U. Spindler, D.S. Jung,
    R. jRadermacher, ASHRAE Trans., Vol. 99,  Part 1, Paper #3655.
                                                                                     69

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  Energy-Efficient Refrigerators
13.  Evahiation ofHFC-134a and HFC-152a as Working Fluids in a Domestic Refrigerator/Freezer,
    J. Pannock, Z. Liu, K. Yu, R. Radermacher, ASHRAE Transactions, Vol. 100, Part 1.

14.  Testing of Domestic Two-evaporator Refrigerators with Zeotropic Refrigerant Mixtures, Bob
    Rose, Dong Soo Jung, R. Radermacher, ASHRAE Transactions 1992, Vol. 98, Pt. 2,
    Paper #3620.

15.  R. Radermacher, "Progress Report to EPA," 1/12/93.

16.  An Experimental Study of the Performance of a Dual-Loop Refrigerator/Freezer System,
    S. Won, D. Jung, R. Radermacher, Submitted to International Journal of Refrigeration.

17.  Experimental Research and Development of a Tandem System Domestic Refrigerator, K. Kim,
    B. Kopko and R. Radermacher, Paper submitted to ASHRAE Transactions.

18.  Development and Testing of a High Efficiency Refrigerator, Q. Zhou, J. Pannock,
    R. Radermacher, ASHRAE Transactions, Vol. 100, Part 1.
  70

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