SEPA United States Environmental Protection Agency Solid Waste and Emergency Response (5306W) EPA 530-F-97-020 August 1997 Waste Minimization: Increased Profits and Productivity Harris Corporation S125K Savings Annually Exempted from CAA and EPCRA Section 313 Requirements Implementing small projects that demonstrated the result- ing savings to management established credibility and opened the door to greater funding for waste minimization What is the Harris Corporation? The Broadcast Division of Harris Corporation manufactures radio and television transmitters. Their manu- facturing process released several hazardous air pollutants and haz- ardous chemicals such as 1,1,1 trichloroethane (TCA), methylene chloride, and methyl ethyl ketone that were used as cleaning solvents, thinners, and degreasers. What Did They Accomplish? Harris implemented a broad range of waste minimization initia- tives that reflect the company's envi- ronmental policy. Harris' savings resulting from all of its waste mini- mization efforts total about $125,000 annually. Environmental Achievements Harris' pollution prevention and waste minimization program is broad in scope and has enjoyed numerous successes... • Alteration of the paint mixing process to a batch process reduced wastes from 1/4 gal- lon to less than a cup per batch, contributing to a reduc- tion in waste paint generation from 3,000 gallons per year to about 900 gallons per year. • Installation of a solvent distil- lation unit also contributed to waste paint reduction. • Replacement of TCA with iso- propyl alcohol during circuit board cleaning eliminated waste TCA. • Replacement of methylene chloride in the vapor degreaser with an aqueous solution elim- inated 25,000 Ibs. of air emis- sions per year. • Implementation of a closed- loop water supply for a spot welder cut water use. • Replacement of an old, larger- than-necessary compressor reduced overall energy con- sumption by 4%. • Replacement of two 45 kw water heaters with a single gas heater slashed energy use. Regulatory Relief Because they eliminated methyl- ene chloride from their vapor degreaser, Harris avoided the need to apply for a Clean Air Act (CAA) Title V Permit and is not subject to Emergency Planning and Community Right-to-Know Act ------- Waste Minimization: Increased Profits and Productivity Harris Corporation (EPCRA) Section 313 requirements. The company is now on its way to being regulated as a RCRA small quantity generator. Also, by not using chlorofluorocarbons or Class I ozone depleting substances, Harris avoided the mandatory labeling requirements under the CAA. The elimination of methylene chloride obviated the need for additional ventilation in the metal finishings room. The Implementation Process The driving force behind imple- mentation of Harris' environmental efforts was a corporation-wide emphasis on the need for quality environmental compliance. As those efforts matured, Harris transited from a regulatory-based approach to waste minimization and pollution prevention, whereby the environ- mental health and safety organiza- tions contribute to the company's bottom line. Harris continuously evaluates its waste streams and processes, and performs annual formal evaluations to develop three-year, rolling strate- gic plans. Pollution prevention and waste minimization efforts are incor- porated into the business unit's overall annual operating plan. The plan is considered a living docu- ment and its goals are subject to change. Current goals are to: • Reduce solid and hazardous waste; • Continue compliance with environmental safety regula- tions; • Reduce toxicity of metal finish- ing chemicals; • Reduce utility costs by 10% per year; and • Increase quality. Most ideas were generated in house. However, when the compa- ny eliminated its methylene chloride vapor degreaser and switched to an aqueous degreaser, it contacted the Illinois technical assistance program for an analysis of available aqueous degreasers. Economics: Costs and Payback Reductions in paint waste have resulted in enough savings to pay for the changes several times over since 1992. Reduction in water con- sumption resulting from implement- ing a closed loop system on the spot welder has saved about $14,000 in water and sewage fees per year, cut- ting the division's annual water costs by 15%. The spot welder pro- ject paid for itself in less than three months. Savings in the electric bill resulting from replacement of the oversized compressor are about $20,000 per year, representing 4% of the division's electric bill. Replacement of the two 45 kw water heaters saves $5,100 per year. Hurdles The biggest difficulty was in securing project funding from upper management. Manager of Facilities and Environmental Compliance Andy Edgar's solution was to estab- lish the necessary credibility for obtaining project funding. He accomplished this by implementing small projects that targeted "easy money" and demonstrated the resulting savings to management. This established credibility and opened the door to greater funding. Words to the Wise Mr. Edgar advises that managers wishing to implement waste mini- mization focus on trying to add value to the company. This helps to keep the projects from being viewed as a necessary evil. In addition, he is a proponent of tapping non-management employ- ees who "...have a thorough knowl- edge of their job, and credible ideas of how to develop and implement improvements." WASTE MINIMIZATION NATIONAL PLAN For more information about the Waste Minimization National Plan, call (800) 424-9346 or check the World Wide Web at http://www.epa.gov/epaoswer/hazwaste/minimize Reducing TOXKS m Our Data's Waste ------- |