v>EPA
/nited States      Industrial Environmental Research  EPA-600/7-78-052b
Environmental Protection   Laboratory          July 1978
Agency         Research Triangle Park NC 27711

EPA Industrial
Boiler FGD Survey:
Second Quarter 1978

Interagency
Energy/Environment
R&D Program Report

-------
                   RESEARCH REPORTING SERIES


  Research reports of the Office of Research and Development, U.S  Environmental
  Protection Agency, have been grouped into nine series. These nine broad cate-
  gories were established to facilitate further development and application of en-
  vironmental technology. Elimination of  traditional grouping was  consciously
  planned to foster technology transfer and a maximum interface in related fields
  The nine series are:

     1.  Environmental Health Effects Research

     2.  Environmental Protection Technology

     3.  Ecological Research

     4.  Environmental Monitoring

     5.  Socioeconomic Environmental Studies

     6.  Scientific and Technical Assessment Reports (STAR)

     7.  Interagency Energy-Environment Research and  Development

     8.  "Special" Reports

     9. Miscellaneous Reports

 This report has been assigned to the INTERAGENCY ENERGY-ENVIRONMENT
 RESEARCH AND DEVELOPMENT series. Reports in this series result from the
 effort funded under the 17-agency Federal Energy/Environment Research and
 Development Program. These studies relate to EPA's mission to protect the public
 health and welfare from adverse effects of pollutants associated with energy sys-
 tems. The goal of the Program  is to assure the rapid development of domestic
 energy  supplies in an environmentally-compatible manner by providing the nec-
 essary environmental data and control technology. Investigations include analy-
 ses of the transport of energy-related pollutants and their health and ecological
 effects;  assessments of, and development of, control  technologies  for energy
 systems; and integrated assessments of a wide-range of energy-related environ-
 mental issues.
                        EPA REVIEW NOTICE
This report has been reviewed by the participating Federal Agencies, and approved
for  publication. Approval does not signify that the contents necessarily reflect
the views and policies of the Government, nor does mention of trade names or
commercial products constitute endorsemeht or recommendation  for use.

This document is available to the public through the National Technical Informa-
tion Service, Springfield, Virginia 22161.

-------
                                       EPA-600/7-78-052b
                                                   July 1978
EPA  Industrial  Boiler FGD Survey:
           Second Quarter  1978
                           by

             J. Tuttle, A. Patkar, N. Gregory, and M. Eckstein

                   PEDCo. Environmental, Inc.
                     11499 Chester Road
                     Cincinnati, Ohio 45246
                    Contract No. 68-02-2603
                        Task No. 36
                  Program Element No. EHE624
               EPA Project Officer: R. Michael McAdams

              Industrial Environmental Research Laboratory
               Office of Energy, Minerals, and Industry
                 Research Triangle Park, NC 27711
                        Prepared for

             U.S. ENVIRONMENTAL PROTECTION AGENCY
                Office of Research and Development
                     Washington, DC 20460

-------
                             NOTICE

     This report,  (prepared by PEDCo Environmental, Inc.,
Cincinnati, Ohio under EPA Contract No. 68-02-2603, Task No. 4)
is provided as an information transfer document.  Data in this
report are supplied voluntarily by industry representatives;
flue gas desulfurization  (FGD) system designers, vendors, and
suppliers; regulatory personnel; and others.  Neither EPA nor
the designated contractor warrants the accuracy or completeness
of information contained in this report.
     Initial distribution of the report is limited to organization
and individuals indicating a specific interest in the field of
FGD technology.  Additional copies of this report and succeeding
issues can be purchased from National Technical Information
Service,  Springfield,  Virginia  22151.

-------
                               TABLE UF CONTENTS




SECTION                                                                                  PAGt


      NOTICfc



      EXECUTIVE SUMMARY                                                                     iv

  1   INTRODUCTION                                                                          l

  2   LIST UF INDUSTRIAL BOILERS  WITH  FtD  SYSTEMS                                           i

           A SUMMARY UF ALL  INSTALLATIONS  BY  NAME,  LOCATION,  STARI-UP DATE, Alvl)
           CURRENT STATUS.

  3   SUMMARY OF FGD SYSTEMS  UN  INDUSTRIAL BOILERS                                          ^

           A BRIEF SUMMARY UF  THE SOURCE  CHARftCTEN 1STICS,  THE CONTROL PROCESS AI\D
           CONTROL SYSTEM SUPPLIEw,  AND  IMFOftMA I IJN ON RECENT SYSTEM PEKFuRMNCe .

  4   SUMMARY BY VENDOR OF FGO SYSTEMS UN  INOUS1RIAL ttUlLERS                               1-5

           A LIST OF THE CONTROL  SYSTEMS  SUPPLIED  BY EACH SYSTEM VENDOR OR MANiJF SCTURER.

  5   OPERATIUNAL FGD  SYSTEMS ON  INDUSTRIAL BOILERS                                        1*>

  6   UNDER CONSTRUCTION FGD  SYSTEMS UN  INDuSIRiAL  BOILERS                                 19

  7   PLANNED F&D SYSTEMS ON  INDUSTRIAL  BUILERS                                             2u

  8   SUMMARY OF DISPOSAL PRACTICES FUR  FGD SYSTEMS ON INDUSTRIAL BOILERS                  ai

  9   PERFORMANCE DESCRIPTION FOR OPERATIONAL F&D SYSTEMS ON INDUSTRIAL BUILERS            35

           AN IN DEPTH DATA  PRESENTATION  FOR THE UPEhATIUNAL CONTROL SYSTEMS.   THIS
           SECTION PRESENTS  BACKGROUND INFORMATION, OPERATING EXPERIENCE,  ECONOMIC
           DATA  , DESIGN DATA, DISPOSAL  PRACTICES,  AND ANY OTHER RELE V ANT  IiMF.uRf>.ft (ION
           AVAILABLE CQrMC-ERWING THE FbD  SYSTEMS  AT  THE VARIOUS  INSTALLATIONS.

  10   DESIGN  INFORMATION FOR  UNDER CONSTRUCTION  FGD SYSTEMS ON  INDUSTRIAL  BulLEkS          9b

           SAME  AS SECTION  9, FOR CONTRUL SYSIEMS UNDER CONSTKlJCTION.

  11   DESIGN  INFORMATION FOR  PLANNED FGO  SYSTEMS ON INDUSTRIAL  BOILERS                    101

           SAME  AS SECTION  9, FUR PLANNED CONTROL SYSTEMS.

  18   DESCRIPTION OF  INDUSTRIAL BOILER FGO SYSTtMS NOT OPERATING                          lUb

            SAME  AS SECTION  t, FOR CON1ROL SYSTEMS WHERE FOR SOME REASON,  1HE  SYSTEM
            IS NOT OPERATING.

  13    PROCESS DIAGRAMS FOR  INDUSTRIAL BOILER FGO SYSTEMS                                  11"?
                                            iii

-------
                                        EXECUTIVE SUN'r-ANY





     1.1E FIRST FULL-SCALE  UMTEP  STATES APPL1CATICN OF FLUE GAb  OFSULFUR I 7 A T I ON (FGD) TECHNOLOGY  TO


['•.'OUST* I Al. FtOTLFRS WAS  AT  1 HE  GENERAL MOTORS PLAiiiT IN ST. LOUIS,  MISSOURI  WHERE TWO FGD SYSTEMS WERE


1NSIALLED ON Tea) COAL.-F IREu  BOILERS IN 147,;.  ]M THIS 
-------
      HIGHLIGHTS FKOM THE CURRENT  INDUSTRIAL PUILEK  FGD  aURVtY  AKF  GlVf.  BEI. Uft:









ALYE'SKA PIPELINE SERVICF CU, HAVE  BfEN OPERATING  A FMC SODIUM  nYORUXIDE  SCKIIttHlNG SYSTEM AT VALUEZ.




ALASKA SINCE JUNK 1977.  THE" FbD SYSTFM KFMOVKS 9f-X  UF SO?  GENERATED  BY  FIRING OIL WITH U.l% SULFUR.




UllhlNG THE REPORT PtRIUO, THE AC ID i C L 1 KlnlM COLLECTED BY  THE M1SI  ELIMINATOR  HAS CAUSED CO"IRUb ION .




I HE PRUHLFM HAS BFtN ALLEVIATED  BY I NC URPOK A I ING  HYPkrtZTNF  SH&AYS  AT  THE  BuTT'l.vi OF THE DEMISIER.









ARCO/PtJLYMERS, INC. HAVE AWARDED A CONTRACT TO FMC FOR A  OUUBLL  ALKALI  FGO SYSTEM TO Bt INSTALLED AT




THE MOMACA, PENNSYLVANIA PLAMT BY  JIJN'F 1980.   THE  THREE  IDENTICAL  BOILERS (. 30u,000 LBS/HR STEAM )




WILL HAVE SEPARATE SC.KUBBEKS WITH  A COMMON  REGENt R A T I (MM  SYSTtM.  THE TOTAL INSTALLED COST OK THE FGD




SYSTEM IS REPORTED TO BE Sb.U MILLIONS.









C.A.M.t A JOINT VENTURE OF UNION CARB10F, AMOCUf  AND MONSANTO,  HAVE ANNOUNCED PLANS TO INSTALL A CO-




GENEkATIQN FACILITY NEAR HOUSTON,  TEXAS.  THE  PROPOSED huO  M«  (FHUIVALENT) POWER PLANT WILL GENERATE




ELECTRICITY AND PROCESS STEAM FOR  THE  EXCLUSIVE USE  OF NEARBY  PLANTS  OF  THE THREE COMPANIES.  THE




TYPE (IF COAL TO BE USED HAS NOT  SEEM DECIDED YET.  HOWEVER  A FliD SYSTEM  IS DEFINITELY UNDER




CONSIDERATION.  THE PLANT IS SCHEDULED TO GO ONSTREAM BY  LATE  1983.









CATERPILLAR TRACTOR CO. CONTINUED  OPERATIONS OF THE  FGD  SYSTEMS AT JOLIET AND MOSSVILLE, ILLINOIS




HLANIS.  THF OPERAIIONAL PROBLEMS  HAVE BEEN HEAVY  FILTER  CLOTH ATTRITION, AND EXCESSIVE WEAR OF  IHE




FGO SYSTEM EQUIPMENT AT THE TWO  PLANTS RtSPFCT 1 VEL Y .









CATERPILLAR TRACTOR CO. REPORTED THAT  <4 FMC DOUBLE ALKALI FGD  SYSTEMS WERE STARTED UP AT E. PEORIA,




ILLINOIS IN APRIL 1978.  THE SYSTEMS ARE DESIGNED  TO REMOVE 90* OF S03  FROM THE FLUE GASES GENERATED




BY BURNING 3.2% SULFUR COAL.  FGD  OPERATIONS PROCEEDED FOR  THIRTY  DAYS  BEFORE THE BOILER PLANT WAS




SHUT DOWN FOR SUMMER.









CHEVERON U.S.A. INC. HAVE REPORTED THE STARTUP OF  3  FGD  SYSTEMS AT THE  BAKERSFIELD, CALIFORNIA OIL




SHE IN JUNE/JULY 197B.  THE SODIUM CARRONATE  SCRUBBING  SYSTEMS WERE  SUPPLIED dY KOCH ENGINEERING AT




A TOTAL COST OF » 2.6 MILLIONS.  EACH  SYSTEM TREATS  FLuF  GASES FROM 6 IDENTICAL OGILERS, WHICH HAVE




A TOTAL RATING OF iOO MM 8TU/HR.   THE  STARTUP  HAS  BEEN SUCCESSFUL.
AT THE FIRESTONE TIRE AND RUBBER cu.  IN  pension, PENNSYLVANIA,  THE FMC DOUBLF ALKALI



PLANT CONTINUED OPERATIONS.   THE SYSTEM  COMPONENTS,  ESPECIALLY THE F.D. FAN AND THE SCKUbHER



INTERNALS, HAVE EXPERIENCED SEVERE FLYASH  ABRASION.   DURING THE  REPORT PERIDO, A NEW FAN HAS PUT  IN



WITH A HOUSING METAL1ZED 8Y 31b SS.   THE MILD  STEEL  SPRAY  hiOoS WE9E REPLACED I1Y 316L So.
THE FMC SODA ASH PLANT IN GREEN RIVER,  WYOMING  REPORIEu THAT  SuS REMOVAL EFFICIENCIES uF 87-9'U




ACHIEVED DEPENDING UPON THE L/G RATTO,  AND  REC IRCUL A T ING LIQUOH PH.  PH VARIATIONS, AND LEAKS  IN  Tup




        WERE THF MAIN OPERATIONAL  PRUBLPKS  DURINi.,  THE  KF.POiVI  Pt^IOD.

-------
                 S  C"kWtf"LV  W**n«l  PSD  SYSUM5  AT FlVt  INSTALLATIONS  AKO.J.MD THE UNI1EO STATES.
     ALLOWING  UPUAIt  INFURMAITUN  WAS PrfOVIOFO  HY   PArtl-'A, 0,110 M)R  THt UOUPLF  ALKALI FGD SYSTEM:
                                        SYSTEM  H*°  AN ^^^ITY  ^ ™*.  ^ ^cu^ AND LiM
                                                                               J^, THE F6D SYS, EH
                           BUNNKEH MILL-  IWIANA kFpOhiTED PLANS FOR A DOUBLE ALKALI FGD SYSTEM, WHICH
 «ILL  TKEAT  FLUE  GASES  FROM  £ EXISTING  ANU  i PROPOSED BOILERS.  THE BIOS ARE UNUEW EVALUATION, AND
 IHt  SYSTEM  IS  SCHEDULED  TO  STARTUP  IN  AUGUST
                              IH TRUN*' C*^^*""!* * SODIUM CARtiONATE SCRUBBING SYSTEM WAS STARTED UP
 AlOMGwiTH  THE  NFft  l.i flM  TONS/YR SuOA ASH PLAWT.  THE FLUE GASES FHOM T«0 ig-M« COKE, COAL, AND OIL-

 FTkEu dOILERS  ARfc  SCKUbBED 8Y THE SODA ASH END-LIHUOrt IN TnO SC^UdflEKS SUPPLIED rtY COBUSTIUN EOT.
 IHt MAJOR  STARTUP  PROBLEM «AS WEAKENING OF THE PUL YPkOP YLEHE SIEVE TRAYS, WHICH WILL BE REPLACED BY
 ilhL SS OR A HIfiHb'i< GRADE ALLOY.
                    C°* KEPOI
-------
                                             StCTTUN   1
                                             INTKOUUCTIOU

    IriJS REPORT ADDRESSES THE APPLICATION UF FLUE GAS  OF rillLF (IR 1 / A T I ON  (FGD)  TECHNOLOGY TU INDUSTRIAL
i:lf)ll.t.*b.  THt NRtl) FU« SuCH A DOCUMENT HAS AKlSEu AS  A  RESULT  UF  MOKE  STRINGENT  EMISSION REGULATIONS
UHblG"EO TU REDDLE SULFUR DIOXIDE.  ISO?) tMlSSIUNS.   IN  VIEW l)F  THF  DEVELOPMENTAL STATUS OF FbD TECH-
,MI:LI.H,Y, EPA'S INDUSTRIAL ENVIRONMENTAL RESEARCH LABORATORY  IN  RESEARCH  TRIANGLE PARK is ESTABLISHING
A PERIODICALLY UPDATED ENGINEERING APPL 1C A T 1 UN/IiMFuRMA T TON  TRANSFER PROGRAM FOR  INDUSTRIAL USE OF
bfld LtlNTROL TECHNOLOGY.
    FI«ST ISSUED  IN DECEMBER 197?  AS  A COMPREHENSIVE  9UO-PAGE RFPOKT ON S0£ CONTROL SYSTEMS ON ALL
           CUMbUSTlOlM AND PHUCLSS  SOURCES, THE CURRENT  StRIFS,  in THE  INTEHFST OF tCUNOMY, AOOKESSES
     TMDUSIRIAL HOlLErt APLICAT10MS OF KGD TECHNOLOGY.   THE  FIRST ISSUE OF THIS SEKIES, ENTITLED "EPA
IMiMJSTnilAL HOILER FGD SURVEY: FIRST JUARTER  l^rfl",  PRESENTED  DETAILED  TECHNICAL INFORMATION ON
INDUSTRIAL BOILERS F&D INSTALLATIONS.  THE INFORMATION WAS  OBTAINED BY A SURVEY OF PLANT PERSONNELr
CONlKOL SYSTEM VENDORS,  REGULATORY AGENCIES,  AND ENGINEERING  FIRMS.
    1ME CURRENT REPORT REPRESENTS  AN  EXPANSION OVER THE FIRST UUARTEK  1978 REPORT WITH RESPECT TO
BOTH   IHE NUMBER  OF  1NSTALLA1 IljNS, AND THE  INFORMATION PRESENTED FOR EACH INSTALLATION.   THE  DATA
ARE GTVF.M IN  TWO  TYPES OF  TABLES:  ONE GIVFS  SUMMARY INFORMATION; THF OTHER, UFTAILED  INFORMATION.
SUMMARY TABLES PRESENT INFORMATION AS FUNCTIONS  OF  TYPE OF  CONTROL PROCESS, CONTROL SYSTEM VENDOR,
OISPuSAL TECHNIQUES  AND  OPERATIONAL STATUS  (OPERATIONAL,  UNDER CONSTKUCTICiN,  PLANNED,  OR  NOT  OPERAT-
ING).   .MUMBEHS, OPERATIONAL  STATUS, AND  OVERALL  CAPACITY  OF THt FGD SYSTEMS ARE SUMMERIZED IN THE
tXtCUTIVE SUMMARY.   UETAILtD INFORMAITuN  INCLUuES:  CONTROL  SYSTEM DESIGN PARAMETERS,  OPERATING EXPE-
RIENCE, ECONOMICS, PROBLEMS  AND  SOLUTIONS, WASTE DISPOSAL TtCHNIUUES,  AND MAINTENANCE  PRACTICES.
    Tut INFORMATION  IN THlb  REPORT WILL  BE PERIODICALLY UPDATED AND EXPANDED  BY MEANS  UF  TELEPHONE
AND MAR SURVEYS, AND  PUBLISHED  EVERY UUAKTEK.   IN  FUTURL REPORTS, THE DATA BASE ON SELECTED  PLANTS
nILL BE EXPANDED  BY  UN-SITE  SURVEYS.   INDIVIDUAL SURVEY REPORTS WILL ALSO BE  PUBLISHED FUR THE
wESPfcC I IVE PLA.MTS.
    CERTAIN  ENGINEERING  SYMBOLS  AND  TERMS  ARE  USED  VERY FREOUENTLY IN THE FIELD OF FGD TECHNOLOGY.
TABULATED BELOtt ARE  THE  DEFINITIONS OF  PERTINENT SYMBOLS AND TERMS USED  IN THIS REPORT.
   SYi'hOL/TtRM                                     DEFINITION
  ACFM               ACTUAL  CUBIC  FEET  PER MINUTE, UNIT OF GAS FLOW RATE fEASURFD  AT  ITS  ACTUAL
                    TtMPErtA IllKE  ANT) F'RESSURE
  AVAILABILITY       HOURS  THE  FbO SYSTEM WAS AVAILABLE (WHETHER OPERATED OR NOT)  DIVIDED BY  HOURS  IN
                    PERIOD,  EXPRESSED  AS PERCENTAGE
  F                  DEGREES  FARENHEIT,  UNIT OF  TEMPERATURE
  F.n.               FuHCEiJ  DrtAFI

-------
   SYMBOL/TERM






  GP>"




  I.D.




  L/G






  OPERABILITY






  PSIG




  RELIABILITY






  SCFM






  T




  rtli




  0/XX
                                 DEFINITION
 GALLONS  PER  MINUTE




 INDUCED  DRAFT
EXPRESSED
                                    LIaU1° FL°" °mDED BY 1ME
                                                                    PERJOD,
POIIIMDS PER SQUAKF INCH, UNIT OF PkESSURE






EXPKESSEO Is°PEKCStNTAGES
                                           *'  HOURS  IT  «S CALLED UPON TO OPERATE,






                                      UF  GAS  FLOW  HAIE  "tAsu«ED AT 70 F ANU i ATM.




TEMPERATURE




WATtR GAUGE, UNIT UF PRESSUKE DKHP EXPRESSEU  AS  INCHES UF f.ATER



WHEN IHt EXACI MONTH OF A STARTUP DATt iS  NUT  AVAILABLE  IT  IS  INDICATED BY A ZERO
    ANYONE DESIRING TO RECEIVE  THE  [lUAKTtRL*  UPDATED  VERSIONS OF THIS REPORT FREE OF COST, MAY




HEUUEST ADDITIUN OF HIS OR HfcR  NAME  IU  THE  MAILING  LIST  BY  CONTACTING THE EPA PROJECT OFFICER UR THE



CONTRACTOR.

-------
                                US! uF iNtJOSTRlAu r.OHERS  /, I T H  tuD  SYSIEHS
                                                                                    blATuS Ab UF 0//3
-------
                                         5t 1. T ION   ? (COM INUEl))


                                 L1S1  OF  INDbSlRlAL bOlLEkb ,< I 1 H Fblt SYS1EMS
                                                                                      STATUS AS OF 07/30/78
 INSTALLATION NAME


 GKEAT  WESTERN SUGAR

 GREAT  WESIEKN SUGAR

 GrtEAT  lut.SIERN SUGAR

 GKEAT  lit SI EKM SUGAR

 GKFAT  ASTERN SUGAR

 GrtrAT  WESTERN SuGAR

 GKloSuw  AIR  FORCE HASE

 HAHKIa MINING CO.

 TIT RAYONIER,  INC.

 KERR-MCGEE CHEMICAL CORP.

 MtAu PAPERBOAKD  CO.

 MINN-OAK FARMER'S COOPERATIVE

 MUHIL  OIL  COMPANY

 MublL  UIL  COMPANY

 NEKOOSA  PAPERS,  ItMC.

 TUAuIfY  MILLS, INC.

 RICKfcNBACKEK  AIR  FORCE BASE

 SHELLtR  GLObE  CORP.

 SI. JUE  ZINC  CO.

 sr. REGIS PAPER co.

 TtXACO INCORPORATED

 TtXACU 1MCORPORATEQ

 TtXASbllLF

TKAfcSCO  TEXTILES,  IMC.

il.S. GYPSUM CORP.
                        LGCATiUN


                    FREEMON1,UHJO

                    GERlNb, NEBRASKA

                    GREEIEY, COLOkAlid

                    LUNGMuMl,  COLORADO

                    LOVELAND,  Cul UPADO

                    SCOI1S DLUFF,  NESitAbKA

                    BUWKEh HILL,  INDIANA

                    SPRUCE PINE,  NORTH CAROLINA

                    FtHNANDlNA bEACH, FLORIDA

                    TKONA, CALIFORNIA

                    SlEVtNSUN, ALABAMA

                    HAHPEION,  NOK'IH DAKOTA

                    BUTTOiMWlLLOw,  CALIFORNIA

                    SAN  AKDO,  CALIFORNIA

                    ASHOOtvN, ARKANSAS

                    MI.  AIRY,  NORTH CAROLINA

                    COLUMBUS,  OhIU

                    NORFOLK, VIRGINIA

                    MUNACA,  PENNSYLVANIA

                    CANTONMENI,  FLORIDA

                    SAN  AROO,  CALIFORNIA

                    SAN  AROO,  CALIFORNIA

                    GRANGER, YiYOMiNb

                    AOGUS1A, UEORUIA

                    OAKMONT, KEfiNSYLVAM A
START-UP
DATE
10-7B
10-75
10-75
10-73
10-73
10-75
9-79
0-73
0-75
6-78
0-75
b-7 I
9-78
0-74
2-7b
5-70
3-7fa
0-75
10-7b
0-73
11-73
,-7b
3-75
0- 0
STATUS*
2
1
1
7
1
1
5
7
1
1
1
1
2
1
1
7
1
1
2
1
1
1
7
7
    PAGE  NUMBER*


 9/(  9,14,19,22)

 &7(  9,14,17,23)

 69(  9,14,17,23)

107(  9,14,  0,23)

 70(  9,14,17,23)

 Vd(  9,14,17,23)

105(10,14,20,21)

108(10,15,  0,24)

 74(10,13,18,23)

 76(10,13,18,22)

 78(10,13,18,21)

 80(10,14,18,23)

 98(10,14,19,22)

 82(11,14,18,22)

 83(11,13,18,21)

109(11,13,  0,22)

 85(11,15,18,22)

 88(11,15,18,24)

 99(11,13,19,22)

 89(11,13,18,23)

 91 (12,13,18,23)

100(12,13,19,24)

 93(12,15,18,23)

110(12,14,  0,23)

111(12,13,  0,21)
* STATUS CuDES
  0 - STAluS NOT DEFINED
  1 - UPEWAT10NAL
  a - CO.MSTRUCTluNAL
  3 - PLANNED-CONTRACT
                                                     5 - PLANNEO-REfJUESl ING/EVALUATING RIDS
                                                     6 - PLANNED-CONSIDERING  so?  CONIROLS
                                                     7 - TtRhlNAIF.ly
                                                     B - luOEFllMITt'LV  SH01  DOWN
                 - PLANNED-LEU fcR  01-  I MEM  SIGNED  9 - NEVER S1AKTEP-UP


             + FOK COMPLETE  INFURNAIIOK  ON I HE  INDICATED FGU SYSTEM REFER  TO  URSI  PAGE LISIEU.
               THE INSlALLAIIuN  APPEArxS  IN uTrlEh SUMMARY bECTIOl.S ON  THE PAGES  IN PARENTHESES.

-------
                                                                                  STATUS AS UF  07/30/78
                                            SECTION   ?

                             bUMMAhY  UF  FGO  SYS1EMS  UN  INDUSTRIAL BUILEKS
CU''1'A;MY TNFURMA1 ION

AlYtS'vA PIPELINE SERVICE CO.
vAi.iiF/, ALASKA
FK: F ,\iVlRuNMENT AL F.UUIPMENT
FiifL UTL  CO. 05% - 0.1X  SULFUR)
•jO.Ully SCFM   (DESIGN  1-iAXlMUM)
MUK 1-up    6/77
SuniU.1-. HYDROXIDE bCKUbtUMG
SIATIIb -  UPERATIUNAL
     tCArJ  THREAD  CU.
     dN, NORTH  CAROLINA
K.:. bLY  MANUFACTURING  CU.
CIIAL (0.8%  SULFUR):  H\TERRUPTIBLE  NATURAL GAS
Iti.jOO  SCFM  (T01AL  -  c  TOILERS)
S1AK1-HP     U/73
CAllsTIC-WASTE  STREAK
SIA1US  -  OPERATIONAL


AKCG/HOLYMERS,  IMC.
MUNACA, PENNSYLVANIA
F«iC  ENVIRONMENTAL EQUIPMENT
COAL li.O*  SULFUR)
aih,oon SCFM (TC1AL - 3 BUTLERS)
SIART-UH     6/80
IHHIi-jLE  ALKALI  (CONCENTRATED)
STAIUS  -  PLANNED-CONTRACT ArtARDED

ARMCU  STEEL
M10ULETOWN,  OHIO
KOCH ENGINEERING
CUAL IU.8*  SULFUR)
HU.uOO  bCFM (TOTAL - i. BOILERS)
S1AKT-IIP     0/7b
LIME bCKUBBING
STAIMo  -  OPERATIONAL

HUNIStf  INC.
CAIhC.  ILLINOIS
 OKAvO  CURP./NAT'L LIMb ASS'M
 COAL I'ii  SULFUR)
 44,iHiU  bCFM (TOTAL - d dOlLtRS)
 S1AKT-UP     9/  0
 Ll"it SCKUH6ING
 STAlilH - TERMINATED

 C.A.M.fCARBlDE-AMOCU-N.ONSAMTOj
 lIUHSTON.  Tt'XAi
 n. u T StLbCTEO
 NuT StLtCTED
 1 ,<>UO,  (i00 SCFM  (1 BOILER)
 SrAhT-UP    10/83
 MUT SELECTED
 SIAllia - PLANNEU-COIMSIDERIWG  $0^  CONTROL
SU"'-
-------
                                                                                  STATUS A3  UF  07/4U/7B
                                      SECTION  3 (CONTINUED)

                              SUMMARY OF  FGD SYSTEMS ON INDUSTRIAL BOILERS
 COMPANY  INFORMATION
                                                     SUMMARY OF KECENT OPERATIONS
 CARBORIJMDUM  ABRASIVES
 BUFFALO,  ME^ YORK
 CARBORUNDUM  ENVIR.  SYS.  LTD.
 COAL  12X  S AVERAGE,  S.iJX  S  DESIGN  MAX)
 36,000 ACFM  3  3bO  F
 SIAKT-UP     O/  U
 LIMt  SCRUBBING
 STATUS -  PLANNED-CONTRACT AwARDhO
NO  DEFINITE  PLANS  HAVE  BEEN  MADE FOR THE CONTnOL
Oh  S02  EMISSIONS FROM  THIS BOILER.   THF FUTuRf UF
THE CONTROL  SYSTEM  WILL  Bt DETERMINER BY A REGU-
LATORY  AGENCY  DECISION  EXPECTED  NEAR THE END uF
197t>.   THE CURRENTLY OPERATING  vENTURI  (L/G = 10)
CONTROLS ONLY  PARTTCOLATE, BUT  TIE-INS  HAVE BEEN
PKOVIOED FOR A  LIME SCRUBBING  SYSTEM USING
A 6-siAGE SPRAY TO. BOILERS)
SIAKT-UH    9/7K
DOIioLE ALKALI  (DILOIE)
STATUS - OPERATIONAL
THE FGO SYSTEM CONSISTS OF  AN  INDEPENDENT
SCR08BING TRAIN ON EACH OF  TrtO  COAL-FIRED  BOILERS.
THESE BOILERS HAVE BEEN OPERATIONAL  EACH HEATING
StASON SINCE OCTOBER  1974.   SINCE  THAT  OATE,
SCRUBBER AVAILABILITY HAS BEEN  AVERAGING ao-s^x.
SEVERAL PROBLEMS PLAGUED 1977-1978 OPERATIONS:
UNRELIABLE 305 MONITORS, HIGH  EROSION OF FILTER
CLOTH, AND PLUGGED PIPELINES.   SLUDGE FREEZING
WAS ALSO A PROBLEM AREA.
CATERPILLAR TRACTOR Co.
MAPLF10N, ILLINOIS
FwC ENVIRONMENTAL EQUIPMENT
COAL 13.2X SULFUR)
li>7,UUO SCFM (TOTAL - 3 BOILERS)
START-UP   10/78
DuilbLE ALKALI (CONCENTRATED)
STATUS - CONSTRUCTION
AT THE CATERPILLAR MAPLETON PLANT,  FMC  CONCENTRA-
TED MODE DOAL ALKALI  TECHNOLOGY KILL  BE  UTILIZED
TO CONTROL S02 EMISSIONS.   [HREE  SCRUBBER  SYSTEMS
WILL START-UP IN OCT. 1978, CONTROLLING  EMISSIONS
FROM THREE COAL-FIRED BOILERS.  CONSTRUCTION
DELAYS, PRIMARILY On  [HE STEAM GENERATION  SIDE,
HAVt DELAYED SYSTEM START-UP BACK  TO  THE  1978-79
HEATING  SF.ASON.  BY  THE EARLY i980's  THERE >VILL
Bt 8 FMC FGD SYSTEMS  AT TriE TrtO MAPLETON  SITES.
CATERPILLAR TRACTOR CO.
MiiMlOw, ILLINOIS
7URr, INDUSTRIES
COAL (3.ax SULFUR)
«U,OOU SCFM (TOTAL -<2 BOILERS)
STAKT-UP    1/78
DOUBLE ALKALI (UILUTF)
STATUS - OPERATIONAL
THE CATERPILLAR MORION PLANT UTILIZED  ZORN  INDUS-
TRIES' DILUTE MODE DOUBLE ALKALI  TECHNOLOGY
TO CONTROL EMISSIONS FROf THE STEAM  PLANT.
FGD SYSTEM START-OP OCCURRED AT  THE  BEGINNING
OF 19/8.  OPERATIONS CONTINUED  10 BE PROBLF
DURING THIS REPORT PERIOD.  SOME  BOILER-RELATED
PROBLEMS HERE EXPERIENCED.
CATERPILLAR TRACTOR CO.
MuSSVlLLE, ILLINOIS
FISC ENVIRONMENTAL EUUIPMENT
COAL (3.ax SULFUR)
140,000 SCFM (TOTAL - 4 BOILERS)
STAKT-UP   10/7S
DOIIHLE ALKALI (CONCENTRATED)
STATUS - OPERATIONAL
THE CATERPILLAR MOSSV1LLE PLANT HAS UTILIZED  AN
FMC CONCENTRATED MODE FGD SYSTEM EACH HEATING
SEASON SIlMCE OCT08F.R 1975.  THERE A«E FOUR  COAL-
FIRLD BOILERS EACH bEING TREAIED BY A SEPARATE
scROBBiuG TKAIN.  OPERATIONS FOK THE 1977-78  HEAT
SEASON WFRE MARKED BY EROSION IN Tut SCRUBBER
LINING, PIPING, PUMPS, AND CONTROL VALVES.
CnFvtKOivi U.S.A. INC.
flAMiiVSFiELt), CALIFORNIA
NUT SELECTED
OIL U.1I SULFUR)
14h,000 SCFM (TOTAL - 1 £ BOILERS)
SlAhT-UP    4/79
SODIUM CARBONATE SCRUBBING
STAillS - PLANNEO-RFtJUcSTING/EVALUATING BIDS
CHEVERON U.S.A. IS PLANNING TO  INSTALL  TWO MORE
FGD SYSTEMS A[ BAKERSHIELO OIL  SHE.  IHESfc WtLL  RE
OivCt.-THROUGH, SODIUM CARBONATE  SCRUBBING  SYSTEMS
AND ARE SCHEDULED TU GO Om-STREAM BY  APxIL 1979.

-------
                                                                                    STATUS AS OF U7/30/7tt
                                      af-cTHi.*   <  icn:.i INHJFJ)

                              SUMMARr UF-' Fbl) SYSTEMS  '"• INDUSTRIAL "BOILERS
        IllFORMAl ION
                                                      SijV'iARY IH- RFCt'NT  ''PFRATTUNS
CHFVRUN U.S.A.  IMC.
SAKtRSFlELU, CALIFORNIA
KOCH ENGINEERING
OIL (l.U SULFUK)
2«tt,00i> SCFM ITuTAL  -  Id  bOiLtRSl
START-UP    7/7h
SODIUM CARBONATE  SCRUBBING
STATUS - OPERATIONAL
                                                      CriK l/RUN U.S.A. HAS  PURCHASED IHwFE FRO SYSTEMS
                                                      FROM KOCH E.iGINcFR I ^G.  THt SOOIuf CAHiiOivAIF  SLrfn-
                                                      rUil.M'^ SYSTEMS JU.M  oN-STREAM IN JUNE/JULY  197n.
                                                      TnF  STARTUP HAS BEE.M  SUCCESSFUL. THt SYSTtMS  ARE
                                                      <'tS lGijf',J Kl REDUCE  SOc  c;'ISSluiMS BEi-O* 7U  PHM.
FIRESTONE TIRE  AND  KUoBER CO
PUTISTO.MN, PFNNSYUVANIA
FIV.C ENVIRONMENTAL EUUIPMENT
?.5-.i.OX SULFUR  CUAL
B07U SCFM (13(OUO ACFh  aj 3(")
S1AKT-UH    1/7S
DOllttLt ALKALI  (CONCF.NTRATEDJ
       - uPERATIOiXiAL
                              F)
THt FbO SYSTEM  AT  FIRtSKlNF-POTTSlOivrM  CONSISTS  UF
AN FML UOU6LE ALKALI  DUAL THUOAT VF.IMTUKI  SCKUBBtR.
Into 30e CONTROL  SYSTtM nAS BulLT AS A  OFMOivSIKA-
T|f)r< HRiUECI F-U.'jDtn  BY  FlKFSlUNt. TM?  SYSIFM  OPt«-
AlEl) rtllri AIM AVAIl.AblLTTY VALUF. OH 91 'I.  IN  THE FALL
UUAnTtW UF  19/7.   Int" MA.lOtt PKUBLtM  AHKA  .lAii
PK05ION OF  FAN  AND SHiVAY NOZZLES aY  FUVASH.  ThE
FAN AiMO SHRY KODS  KtSt  KFPLACen KM APRIL  1 <* IA.
FMC (SODA ASH PLANT)
GKF.tN RIVER, WYOMING
FrtC ENVIRONMENTAL  EUUIPMENT
CliAL (1% SULFUR)
4«b/UUO SCFM  [TUTAL  - 2 BOILERS)
START-UP    5/76
SUIHUM CARBONATE  SCRUHBiMG
STATUS - OPERATIONAL
                                                      THE FGO SYS1EM  CONSISTS fiF TftO FMC SODILJN1  SCRufl-
                                                      HlNb UMTS  TO Rt^OVh  SULFUR UIOxIOE A.MlJ  HARTICU-
                                                      LATh HATTtR FROM  1Ht  FLUF GAS OF  I WO BOILERS.
                                                      SCRUBBER UIKROSION  HAS KFtfM A PROBLEM.   PLANT
                                                      PERSONNtL FtLt  THAT THE LINING rtAS IMPRuPERLY
                                                      APPLIED.  FOAMING  AND SEDIMENTATION HAS  OCCURED
                                                      IN I HE SCRUBBER DUE TU ICPURI TIES IN tlifc  LluUOR.
                                                      Ph VARIATIONS AND  DAMPER LEAKS ARE OTHER  PRuBtEMS.
GENERAL MOTORS  CORPORATION
DAYTON, OHIO
ENTOLETER,  INC.
COALfO.7% - 2.OX  SULFUR)
36,000 SCFM (TOTAL  - d BOILERS)
SIART-UP    9/71
SUDItlM HYDROXIDE  SCRUBBING
STATUS - OPERATIONAL
                                                      THF FGI.) SYSTEM  CONSISTS OF IWU ENTOLtlhR  SODIOM
                                                      HYDROXIDE SCRUBBING UNITS. THE UNITS  HAVE  BEEN
                                                      UPHKATIONAL  SINCE  SEPTEMBER H7t.   1 Ht  AVERAGE
                                                      OPFKABILIIY  OF  THE SYSTEM IS S5*. THE ORIGINAL
                                                      31hL SS MIST  ELIMINATORS ARE SEvERLY  CORRODED, AMU
                                                      'ULL bF. REPLACED  BY HAS1E ALLOY-G.   PLUGGING  OF RF.-
                                                      CIRCULATTON  LINES, CAUSED BY FLYASH,  HAS  BEEN A
                                                      SERIOOS PROBLEM.
GENERAL MOTORS  CORPORATION
PARf.A, OHIO
Gl'l ENVIRONMENTAL
CuAL  (H.5X SULFUR*  7.1* ASH«
1^8,100 SCFM a)  70  F (TOTAL -
START-UP    V71
DuubLE ALKALI  (OTLUIE)
SVATUS - OPERATIONAL
                              l?,^b(i BTU/LB)
                              1 BOILERS)
THE FGO  SYSTEM  CONSISTS OF 4 GM-DESIGNED   DUUBLE
ALKALI SCRUBBERS  UPERATIO.MAL ON a BOILERS.   THE
SCRU8BEKS  HANDLE  A I01AL d1d,00o ACFM  OF  FLUE GAS.
THF SCRUBBF.RS HAVE BFEN OPERATIONAL  SINCE MARCH
1974.  THE  SYSTEM HAD AN AVAILABILITY  OF  78*
DURING THIS  REPORT PERIuD.  FILTRATION EQUIPMENT
AND LIME SLURRY FEEU PUMPS rtlLL BE REPLACED.
GENERAL MOTORS  CORPURATION
PUNTIAC, MICHIGAN
PEABUUY ENGINEERING
CUAL  (0.84%  SULFUR)
Iu7,300 SCFM (TuTAL -   F K'FHEAT.

-------
                                                                                    STATUS  AS OF  07/30/78
                                       bf.CTIOr-.  5 (CONTINUED)

                               SUMMARY  oh  rb n  SYSTEMS ON INDUSTRIAL BUILERS
         INFORMATION
                                                      SUMMARY OF RECENT OPERATIONS
 I'ft.KAL MOTORS CORPORATION
 TliMljAAr.i[,A, |\,Fft YOKK

 FM; F\V1RONMFNTAL EljUIPMEiMT
 COAL. (1.3% SIILFuR)
 3e,,M)l)  aCFM (TOTAL - '4 HOILERS)
 START-UK    h/7b
 Sol/Ill:1-'  riYORUXlOE SCRUBBING
 SI ft [lib  - OPERATIONAL
                                                      THE  Flit) SYSTEM CONSISTS OF FOOR GM  SOOIOM  SCRUR-
                                                      rtlM, UNITS FOR THE REMOVAL UF PARTICULATES  AND
                                                      SULFUR  DIOXIDE FROM FOUR COAL-FIRED BOILERS.
                                                      IMF.  SCRUBBERS ARE EQUIPPED WITH VENTURI  SCRUBBERS
                                                      FUR  PARTICULATE REMOVAL.  UNSTABLE  PH CONTROL,
                                                      PIPE EROSION AND STACK CORRISION ARE MAIN  PROBLEM
                                                      ARFAS.   REPLACEMENT OF CONTROL SENSORS,  PIPING
                                                      Awn  RELINI.MG OF STACK ARF. THE CORRECTIVE ACTIONS.
                 PAPER co.
 L'KiisSt T I ,  ARKANSAS
 ' IKPI'L  INDUSTRIES
 ^Arvis  A..JU  OIL UR COAL u* - i.i% SULFUR)
 2,000  SCFM (1 BOILER)
 SFART-UP     0/7!i
 CAUSTIC  WASTE STREAM
 STATUS  -  OPERATIONAL
                                                      THE  FGD  SYSTEM CONSISTS OF AN AIR-POL CAUSTIC
                                                      SCRUBBING  UNIT TO REMOVE SULFUR DIOXIDE AND PAR-
                                                      UCULATE MATTER FROM THE FLUE GAS OF A COAL/BARK
                                                      OK UIL/BARK  POWER BOILER.  [HE SYSTEM IS PRECEDED
                                                      BY CYCLONES  FOR PARTICULATE REMOVAL.  DURING THE
                                                      REPORT PERIuD  No MAJOR PROBLEMS OCCURRED.  THE
                                                      BOILER-SCRUBBER HAS BEEN OFF-LINE A TOTAL OF ABOUT
                                                      Ib OAYS  SINCE  JANUARY.  GLASS LININGS IN THE
                                                      SCHuBdEK ARE REPLACED AS THEY FAIL.
 GETTY  OIL  COMPANY

 r»AKhPSFlELO,  CALIFORNIA
 Fi-.C  ENVIRONMENTAL  EuUlPMENT
 CuAL  (1.1% SULFUR)
 7d,uO(l  SCFM (TOTAL  - fe BOILERS)
 S1AKT-UH     b/77
 SuI'lUw  CARBONATE SCRUBBING
 STATUS  - OPERATIONAL
                                                     THF  SODIUM  CARBONATE SCRUBBING FGD SYSTEM WAS
                                                     RETROFITTED  BY  FMC  IN JUNE 1977.  THE SYSTEM HAS
                                                     S02  REMOVAL  EFFICIENCY OF 9UX.  THE MAJOR MODIFI-
                                                     CATIONS  HAVE BEEN REPLACEMENT OF MESH DEMISTER BY
                                                     CHEVRON  TYPE AND  ADDITION OF A KOCH FLEXITRAY IN
                                                     TOP  SECTION.  SEVERAL TYPES OF PH CONTROLLERS ARE
                                                     CURRENTLY UNDER TESTING.   MILD STEEL RECYCLE PIPES
                                                     WILL BE  REPLACED  BY  316L  SS.
BETTY OIL  COMPANY
>)AKERbFIELO,  CALIFORNIA
PiVOPKl AT ARY DESIGN

CRUDl- UiL  (1.1%  SULFUR)

99?,7bO  SCFM  CTUTAL-72 BOILERS)
SIART-IIP   12/78

SODIUM CARBONATE SCRUBBING
STATUS - CONSTRUCTION
                                                     GETTY OIL COMPANY  HAS  DESIGNED •* MORE SODIUM
                                                     CARBONATE SCRUBBING  FGD  SYSTEMS IN-HOUSE.  EACH
                                                     SYSTEM, ONLIKE  THE OPERATING UNITS,  WILL HAVE A
                                                     SCR08BFR PURCHASED FROM  KOCH CONTAINING 3 FLEXI-
                                                     TRAYS AND i FLEXTMESH  DEMISTER.  EACH SCRUBBER
                                                     MILL TREAT GASES FROM  8  ROILERS.  CONSTROCTION IS
                                                     IN PROGRESS AND STAKTUP  IS  DUE DECEMBER 197b.
GKF.AT SOUTHERN PAPER  CO.

CtOAR SPRINGS, GEORGIA
AiSHOL INDUSTRIES

tURK ANu COAL OR OIL  (l.OX-a.UX  SULFUR)
'Jc'O.OuO SCFI«!  (TuTAL - 2  BUILERS)
STAKT-tJP    0/7b

CAUSTIC WASTF SfREAM
SIAIliS - OPERATIONAL
                                                     THE FGD SYSTEM CONSISTS  OF  TWO  AIR-POL CAUSTIC
                                                     SCRUBBERS TU CONTROL  PARTICULATE  AND SULFUR DI-
                                                     OXIDE FROM TWO POWER  BOILERS.   THE  PRIMARY  FUEL
                                                     IS BARK/COAL (BARK/OIL  IS FIRtD OCCASIONALLY).
                                                     THE FoLLOnliMG PROBLEMS  HAVE  BEEN  ENCOUNTERED!
                                                     EROSiuN AND PLUGGAGE  OF  THE  PH  PROBES, INTERNAL
                                                     WEAR ON PUMPS, AMD EROSION  IN THE RECIRCULATION
                                                     LINES.
SI
      ntSTFRN SUGAR
      GS, MuNTAiMA
  EAT me. STERN SUGAR
     10. TU SULF'u&J
  ,UUU bCFM H 70 f
  Ai
-------
                                                                                     STATUS AS UF  0?/iO/7a
                                       SEL.T IPi\  5  (CO.-1 ItMUFD)

                              SUMMARY  OF  FbD SYSIFHS  UN  INDl'STHlAL HuILFRS
ClJ"t>ANY  INFORMATION
                                                       SuMWAKY Of  RFCENT  OPFRATtuNb
b«f AT .vcSTFRN  SUGAR
FiilH -iiiKGAN,  COLORADO
Rht-AT •JtSIERfJ  SUGAR
CoAL I 1.2%  SULFUR,  AVERAGE)
hti.cio SCFM  UOIAL  - 2 BOILERS)
STARf-UP    10/7b
ANKUNIA-LADtN  PROCFSS WATER
8 I AIIIS -  uPtRAT IONAL
ThF VENTUKY  SCRUBBER «AS DESIGNED  FOR PARTICIPATE
CONTROL AND  si ANTED IN ociVft.  rut  CONOENSATE
PKMCESS WATtW  USE l) HAS A HUiH PH  18.7)  AHiCH
WtMUVhS SuMt  S(V.  TnK PARIICULATE  AND SU? CON1RUL
EFFICIENCIES  AKL  4fe* AML) 4SX r(EbHtC T I V F. L Y .
KhFAT v.tSIFKN SUGAR
FHFt-'ONI ,UH1U
lirftAT AtSTEKN SUT,A«
CulL  I U  SlILFUH)
Uu.uOu  SCFM  'ulM»-LADEN PROCFSS  WATtR
 SI AIDS - UPERATIONAL
 GRFAT WESTERN SUGAR  IISFS CONOENSATE PROCESS  WATER
 PRIMARILY FOR PARTICOLATF CONTROL.  THE  WATER
 HAS  A HIGH PH (a.7)  BUT  THE SYSTEM HAS A  LOW soa
 REMOVAL. THE SCRUBBERS  wFRE INSTALLED  IN  OCT'7«.
 PLANT OPERATES OMLY  DORING IHE FALL QOARTER.
 Rwt-AT WESTERN SUGAR
 hLi>nb LlLUFF, P»
 r,RFttr ''VtSTEKfJ SUGAR
 CuAL U.2X SULFUR,  AVtRAGt)
 h'j.e'iu SCFM  (TOTAL  -  d bOlLfcRS)
 olAnT-UP   10/7b
 AM'-uJNIA-LADEN PROCESS ,-*ATtR
 SIAIUS - OPERATIONAL
 THF  PLANT OPERATES  ONLY OORING FALL  UOARTER OF
 EACH YEAR. I HE.  VENTuRI  SCRUBBER WAS  DESIGNED FOR
 PARIICULATE CONIROL AND WAS SIANEO  IN  OCT'7S. THE
 PAKTICULATF AND  Su
-------
                                                                                   STATUS AS OF 07/40/7H
                                       SEcTlOM   3  (CONTINUE!))


                              SUMMARY  uF FGO SYSTEMS  DIM  INDUSTRIAL  BOILERS
 COMPANY INFORMATION


 GRISSOM AIR FORCE BASE
 BDfv'RfR HILL, INDIANA
 NUT SELECTED
 CuAL (0.9% - 4.6% SULFUR)
 ?d,ooo SCFM (TOTAL - i BOILERS)
 S1AHT-UP    9/79
 DOUBLE ALKALI (CONCENT RATED)

 STATUS - PLANNEO-REUUESTING/EVALUATING BIDS

 HARRIS MINING CU.
 SPRuCt PINE, NORTH CAROLINA
 W.to. SLY MANUFACTURING CO.
 COAL 10.at SULFUR)
 1,000 SCFM (TOTAL - Z BOILERS)
 STARI-UP    0/7JS
 WATtP SCRUBBING  (NA.NH3 OPTN.j
 STATUS - TERMINATED
 SUMMAKY OF RECENT OPF_RAIIUNS

 THE AIR FURCE HAS INITIATED A PROJECT  HHICH  WILL
 ADO OIME Nt« COAL-FIXED BOILER TO  THE EXISTING
 SIFAM PLANT.  A PORTION OF  IHE PROJECT  INCLUDES  SIM
 FGD SYSTEM FOR IHE NEW BOILER AiMO ffiCI  EXISTING
 UMTS.  THF A-E FIRM, FOSOICK AND HILMER, HAS
 SPECIFIED A CONCENTRATED DflOHLE ALKALI  FGD SYSTEM,
 A.MO BIDS ARE CURREMLY sFING EVALUATED.  PROJECT
 COMPLETION IS SCHLDOLED FOR AOGUST JO,  1979.

 THE FGD SYSTEM CONSISTS OF A «.«. SLY  IMPINJET
 SCRUHBEK CURRENTLY BEING USED STRICTLY  AS A  PAR-
 TICuLATE CONTROL DEVICE.  THE SYSTEM HAS THE
 CAPABILITY OF SCROrtBIiMG WITH AMMONIA OR CAOSTIC
 IF  NECESSARY.  HOfttVER, AS LONG AS CURRENT
 LOK'-SJLFUh COAL SUPPLIES LAST,  THERE IS No NEED
 FOK soi CONTROLS.
 ITT  RAYONIEH,  INC.
 FLf/.MANDINA  BEACH,  FLORIDA
 AIRPOL  INDUSTRIES
 BARK  AND  OIL  (?x -  d.b*  SULFUR)
 201,000 SCFM  (TOTAL -  Z  BOILERS)
 STAkT-DP    0/7b

 SODIUM  HYDROXIDE SCRObBING
 STAIOS  -  OPERATIONAL
 AT  FERNANDIIMA  BEACH,  ITT RAYONIER FIRES BARK
 AND  OIL  IN  TWO OF  THF FuUK PROCESS STEAM BOILERS.
 PARTICOLATE  AND SO?  EMISSIONS AXE CONIROLLED IN
 TwO  AIRPOL  SCRUBBING  TRAINS.   THE PLAmT HAS PERMA-
 NtNTLY CONVERTED FRuM WASTE  STREAM CAUSTIC SCRUB-
 BING  TO  A SODIUM HYDROXIDE CONTROL.  APPROXIMATE
 SCRUBUER OPERA8ILITY  SINCE JAN.  HAS BEFN 95x.
 KERK-wCGEE  CHEMICAL  CORP.
 TRONA, CALIFORNIA
 CoHoUSTIOiM  EQUIPMENT  ASSOC.
 CuKE,  COAL,  OIL  (O.b%  -  5X  SULFUR)
 7db,000  ACFM a) 320 DEGREES  F
 STAHT-IIP     6/7fl

 SODIUM CARBONATE SCRUBBING
 STATUS - OPERATIONAL
 THE FGO  SYSTEM  CONSISTS  OF  A  COMBUSTION EQUIPMENT
 (CEA)  SUOA  ASH  SCRUBBING  SYSTEM  WHICH REAVES FLY-
 ASH AND  SOLFOR  DIOXIDE FROM THE  FLUE  GAS OF TWO
 COAL-FIRED  BOILERS.   THE  SYSTEM  WENT  uM STREAM IM
 JUNE.  THE  BOILERS  HAVE  USED  UP  To bO< COAL FEED,
 AND 100% UIL FEED.   PULYPROYLENE  1RAYS rtILL BE
 REPLACED BY 316L  SS  OR A  HIGHER  GRADE ALLUY.
MEAD PAPERBOARD  CU.
STEVFNSUN, ALABAMA
AIRPOL  INDUSTRIES
OIL  (l.b% - in SULFUR)
100,1100 ACFM al 450 F  (TOTAL - 2  BOILERS)
SIAwT-up    0/7b
SODIUM  HYDROXIDE SCRUBBING
STATUS  - OPERATIONAL
AIRPOL INDUSTRIES HAS  SUPPLIED  A  PARTICULATE
AND so? CONTROL  SYSTEM FOR  THE  TUQ  OIL-FIRED
BulLEKS AT THIS  MEAD PULP MILL.   DUKliNG  A  JONE
POLP HILL SHUTDOWN, THE  RUBBER  LINER  IN  THE
ABSORBER WAS REPAIRED.   ALSO, MODIFICATIONS WERE
IMPLEMENTED AT  THE  ABSORBER  MOOOLE  INLET  WITH  THE
INTENT OF PREVENTING FLY ASH ERROSION  IN  THE
MODULE.  FGO SYSTEM OPFRABlLlTY WAS REPORTED  TO
PE 100%.
MINN-DAK, FARMER'S COOPERATIVE
WAHPFTON, NORTH DAKOTA
KOCH ENGINEERING
LIGNITE  (1.0% SOLf-UR)
160,000 ACFM a) 450 F (TOTAL - t BOILERS)
STAKT-UP    b/77
A;lMuNIA SCRUBBING
SIATOS - OPERATIONAL
KOCH ENGINEERING HAS SUPPLIED  TmO  AMMOM A-B ASED
S02 CONTROL SYSTEMS FUR  THESE  COAL-FIREO  BOILERS.
EACH YEAR THE PLANT ONLY PRODUCES  SOGAR  DURING  THE
SEPT. - Ft*. PEKIOD.  THEREFORE,  THE  SCRUBBER DID
NOT OPERA1E DURING THIS  REPORT PERIOD.   THE  PLANT
HAS MADE SOME FGO PROCESS MODIFICATIONS  DURING  THE
SCHEDULED SHUTDOWN.
MOHIL OIL COMPANY
BOT10,M«ILLOH, CALIFORNIA
HtATER TECHNOLOGY
OIL (1.1% SULFUR)

Id,000 SCFM (TOTAL - 7 BOILERS)
SIAWT-UP    9/78

SuOlUM CAWBONATE SCKUBB1NG
SIAIuS - CONSTRUCTluN
MOBIL OIL HAS PURCHASED SEVEN EUUCTOR SCROHBERS
FROM HEATER TECHNOLOGY FOR THE CONTROL OF
EMISSIONS FROM I STE4M GENERATORS! d5 MM 8TO/HN).
EACH SYSTEMS CONSISIS OF A VENTURI SECTION,  A
RECYCLE T«NK, AND AN OUTLET OuCT HIIH A MIST
ELIMINATOK.  START-UP IS SCHEDULED FOR SEPT.  1978.
                                               10

-------
                                                                                   STATUS AS UF i)7/3u/7b
                                      SECTION  5 (COMT if(UF'J)

                              SUMMARY  UF  Fb') SYS I EKS OIM INDUSTRIAL  BOILERS
COMPANY INFORMATION
                                                     SUVMARY OF  RECENT  OPEhAITUNS
'•'OBIL OIL COMPANY
SAN AROO, CALIFORNIA
MutUL OIL COMPANY
OIL C2.0X - 2.?S%  SULFUR)
182,000 SCFM  (TOTAL -  JO  bOlLEHS)
START-UP    0/7<4
SODIUM HYDROXIDt  SCRUBBING
S1AIUS - OPERATIONAL
MUBll HAS  ntSIGNFl)  THt H-U) SYSTtM BY IN-HOUSE
FmfilNtF.Klnl'.  ri«Sti>  ON A PAH«|TE.U SODIUM HYDHUXIDE
SCRUBBING  PROCESS.   CUWKi'lSIJN OF MST FLlM.MATQR
ANIl  l.n. FAN  BLAOES HAVt BE'tN ThE MAJOR PrtOltLEM
Awe AS.   TrlF  Su3  REMOVAL EFFICIENCY  IS CHANGED  BY
ADJUSTING  Irifc  PH OF IM.hr LIQUOri.
NtKOMSA PAPERS,  INC.
ASHOOM, ARKANSAS
AIRPfJL  INDUSTWItS
COAL  (U-l.bX  SOLFUHI
211,000 SCFM a) JS55  ^  (TOTAL - 1  HUILEK)
STAH.T-UP    2/lb
CAUSTIC SCRUBBING
STATUS  - OPERATIONAL
 IMF.  FGI.1  SYSTEM CONSISTS OK TWO AIK-POU CAUS1IC
 •SLiioduF.KS  CONl ROLL INS KLYASH ANu SUuFOR  DIOXIDE.
 TME  PLAN!  aePOKTEu NO MAJOH HsoaLtMS FIIK
 Pt^IOi).   SCKOriflLi* HuUKS vATLritil FJUlLF.rf
 (vAS OPERATING  AT
 f>OX  CAPACITY.
QOALIIY MILLS,  INC.
Ml. A1WY,  NORTH CAROLINA
COMMEKCIAL FABRICATION & MAC
FuEL  OIL

STAKT-UP     5/70
WATEW SCRUBBING
STATUS -  TERMINATED
 THIS  SMALL INOU3TKIAL BOILES UTILIZED  A
 CUMMEKICAL FAdWICATIOiM AND MACHINE  ICFM)  SCKUB-ATK
 SYSTF.i-l TO CO^frtOL EMISSlil.vS FSOM  1HE  COAL-FIRED
 SUILEW FROM MAY 1S7U It) DtCEMbdH  1973.
 AI  1HAT TIMt IHEY CONVEKftn TO  FINING  LOW-SOLFUk
 OIL,  REMOVING Trib NtFO TO CONTROL  EMISSIONS.
 RICKENBACKEK AlK FOkCt BASE
 COLUMIIS,  OHIO
 RtSEAHCH-COTTkELL/BAHCO
 COAL  (1.0X SLILFUS)
 50,000  SCFM (1 bOILEHJ
 START-UP     3/7b
 LIMtSTONE  SCRUBBING
 STAIUS  -  OPERATIONAL
 THIb KESFARCH-COTTRELL/BAHCO  LIME  FGD UNIT
 WAS FIRST PLACED IN SERVICE ^ARCH  11, 197b.
 ThF. SYSTEM rtAS SWITCHED  OVER  10  LIMESTONE IN APRIL
 1*7?,  AND HAS REGAINED  IN  THAT  OPERATING MODE Tu
 DATE.   DURING THE SECOND QUARTER OF  1^78, THE FiiD
 SYSTEM HAS DEMONSTRATED  AN OPERABILITY OF 100%.
 THF PLANT REPORTS NU  REMAINING  PROBLEM AREAS.
 SHELLER  GLOBE CORP.
 NORFOLK,  VIRGINIA
 W.W.  SLY  MANUFACTORING CO.
 COAL  (.LESS THAN 1X SULFUR)
 8,000 SCFM (TOTAL - I BOILERS)
 START-UP     0/75
 SODIUM HYDROXIDE SCRUBBING
 STATUS -  OPERATIONAL
 AFTER SYS1EM WE3IART  IN  OCTOBER  1S77,  THERE HAVE
 BEEN NO PKOHLEMS RESULTING  FROM  EITHER BOILER OR
 SCRUBdFR UPtRATIONS.   THE  PLANT  UNOtri  wtNT A
 VIRGINIA EPA INSPECTION  AND WAS  FOUND  TO BE IN
 COMPLIANCE rtlTH THE PARTICULAR  EMISSION REGULA-
 TIONS.
 ST.  JOE ZINC CO.
 MONACA. PENNSYLVANIA
 BUREAU UF MINES
 COAL (i?.5%-4.5X SULFUR)
 10-4,000 SCFM (TOTAL -  1 BOILER)
 S1AHT-UP   10/78
 CITRATE PROCESS
 STAIUS - CONSTRUCTION
.CONSTRUCTION CONTINObS  ON Trit CITRATE PROCESS
 SCHUBrilrtG SYSTEM  WHICH  rtlLU CONTROL So? EMISSIONS
 FROM A bO-Mrt  (NOMINAL  PtAK CAPACITY) COAL-FIRED
 POWER GtNERATING  UNIT.  STARTUP WILL Be OCT'78.
.THIS SYSTtM WILL  riF  ALSO r(FPORTtD IN I HE EPA/PEUCO
 LIIILTTY FliD SUSVEY,   blwCE INFORMATION WILL BE
 GATHERED UURING  THE  ONE YtAK DEMONSTRATION PtKlon
 BY FOLLOWING  A  TYPICAL  UTILITY OPERATING LOAD
 PROFILE.
 ST. REGIS PAPER CO.
 CANlONMtNT, FLORIDA
 AIRPOL INOUSTKlfeS
 BARK AND GAS OR OIL  (LESS  THAN 1% SULFUK)
 115,000 SCFM (1 80ILE«)
 START-UP    0/73
 CAUSTIC SCRUBBING
 STAIUS - OPERATIONAL
 AIR-POL  HAS  SUPPLIED THt CAUSTIC SCKIMBING KG I)
 SYSlErt  TO  kEMOVt  PArtTICdLAIc AND S>Ui_FOK OIOxIoF
 FrIOM  THt FLOE  GAS OH A HAWK BOlLEKi WHICH CAN  ALSO
 FIRE  NATURAL GAS  AND JlL.  PLANT HAS NOT YET
 THt FtED i-.ATEK SOuRCF TO ALuflVlATE PROrtLEMS  OoF
 TO FlttFRS  PLUbGINo LluFS AND MloT FL I.'ilNO I OR.
 PLANT  INDICATED THAT THIS RtPoRT HAD PREVIOUSLY
 RtPORlhi) 1 HO HIGH A FUEL SULFurf CuNlK.MT.

-------
                                                                                    STATUS AS OF 07/iO/78
                                     .  SECT ION  i  (COIMT INutU)


                               SUMMARY  UF Fl,P> SYSIFMS'OiM  i NljUSTh f Al_  BOILERS
 CO'-IPANY TNFORhAT ION

 1EXACU INCUKPURATED
 SA«i ARDu, CAt IFliRiMA
 CEILCdTt
 OIL U./Z SULFUR)
 ieh,ciuo SCFM (TOTAL - 2(4 BOlLtRSl
 SIA.RT-i.JP.   11/73
 SODIUM HYDROXIDE SCKUbBlNb
 SI ft HIS - OPERATIONAL

 TEXiiCu INCORPORATED
 SAN AKIIU,  CALIFORNIA
 DuCuM  COMPANY
 "IL (1.7% SULFUR)
 117,000 SCFM (TOTAL - 9 BUILERSJ
 STAKT-Up    3/79
 SuDUlH CARBONATE SCRUBBING
 -SIATlib - CONSTRUCTION

 lEXASbULF
 GRA,,RtP.f  WYOMING
 Snh-iCU INC.
 dJL (1.1X  SOLFUR)
 ltd,000 SCFM (TOTAL - Z BOILERS;
 S 1 A R T-11P    9/76
 SU01U", CARBONATE
 SIAtUS -  OPERATIONAL

 TSAKiscn TEXTILES/ INC.
 AUGUSTA, GEORGIA
 FwC ENVIRONMENTAL EQUIPMENT
 FOF.L OIL  (.?.%  MAX. SULFUR)
 SO.oOO  ACFM
 SIAKT-IIH     i/7b
 SODIUM  CARBONATE SCRUbSING
 STATUS  - TERMINATED
 SUMMARY OF RECENT OPERATIONS

 EACh FGl) SYSTEM CONSTSlb  JF  A  riORi^UNIAL,  HACKEO-
 RtD SCROBMFR FtIR tACH OH  THE OlL-HREO bOILERS.
 POOR oCKUBBlNii LI.JUOR QUALITY  CAUSES  PLUGGING OF
 PAC^ElJ isEuS AMD SPRAY NOZiLES.   THE SYSTEMS HAVE
 HIGH MAINTENANCE REUtilREMENTS  AND  RELATIVELY LOW
 SO? REMOVAL (73*).  TEXACO  IS  PLANNING TO  PHASE
 HUT THIS (,KOUP OF SCHOHBF.RS BY  LATE 1979.


 TEXACO is PLANNING TO PHASE OUT  THE EXISTING FGD
 SYSTEMS AT THEIR SAN AROO,  CALIFORNIA  OIL  SITE.
 AS THE FIRSl  STEP OK Trit  PROGRAM,  9 OF THE PRESENT
 31 SCrtUbBtKrs UN 50 MM BTU/HR STEAM GEiMERATORS ARE
 BtlivG RtPLACEO bY A MtW SYSTEM,  SOPPUIEO 8Y DUCON
 COMPANY.  THE  Ntw'FGI) SYSTEM WILL  CONSIST  OF THREE
 TRAINS OF A VENTURI SCROHHER/SPRAY ABSORBER COM8I-
 NATIOiM.  THE  SYSTEM IS UNOER CONSTRUCTION.

 THTS SOUIUM CARHONATE SCRUBBING  SYSTEM WAS  DESIGN-
 ED 6Y SrvEMCU.   SOd ABSORPTION OCCURS  IN THE
 QJfc-,«CHfR ANO  THE SIEVE-TRAY AdSORBER MODULE.   AN
 iNTtRtSTING FEATURE IS AN INTERNAL OANPER  WHICH
 ALLOWS A n TO  i  TURNDOWN RATIO.  INITIAL PROBLEMS
 INCLUDED PLUGGING CAUSED aY FLYASH, AND CORROSION
 Iiv RECIkCOLATlON PIPING, CAUSED BY THE SLIGHTLY
 ACIDIC SCRUBBING LIUIJOR.

 THE  Fan OPERATIONS  HAVE  BEEN TERMINATED FOR  AN
 INDEFINITE  PERIOD.   THE  PLANT BURNS NUMBER  6  FUEL
 OIL  AND THE SULFUR  oiuxine EMISSIONS ARE 5
-------
                                                                                   STATUS  AS  UF  07/.*(>/7 8
                                            SECTION  4

                        SUMMARY BY VF.NIH'R  Of-  FGu  bYbltMb UN  INHUSTH1AL
vFhJ'UH
rt.li. I JTTLt
       INDUSTRIES
BUREAU  OF  MINES


CARBORUNDUM ENvTR. SYS. LTD.


CEILCOTF


COMBUSTION EQUIPMENT ASSUC.


COMMERCIAL FABRICATION *  MAC


L'WAVU  CORP./NAT'L LIME ASS'N


ullCON  COMPANY


bfvlOLtlER, INC.


F-'-*C  ENVIRONMENTAL EQUIPMENT
                                      INblALLATTuN NAMt / LOCAIIUN
GFNFhAL M01OKS  CORHOHATIllN
SI. LdOlbt M1SSOUKI

bf UfblA-PACIHL HAPt.K CO.
CHuSbt I T,  AK^AwSAS

liKLAl  bOUTnt-KN  PAPtR CU.
CEUAK  SPKll>gRS,  GtORGIA

IT! KAYOhlEW,  INC.
f-FKNANDIlvA RtACH
                                      Mt AD  PAPtRBDARU CO,
                                      STtVtNSON, ALABAMA
                                              PAPEKS,  INC.
                                      ASrlilOWIMf AKKANiiAS

                                      ST.  Ktblb PAPEK  CO.
U.b.  GYPSUM COKP.
UAHMUNT,  PENNSYLVANIA

bT.  JOE  ZINC CU.
MONACA,  PENNSYLVANIA

CARBORUNDUM ABKASIVES
dllFFALOr  NtW YUKK.

TF.XACO  INCOKPOKA1FU
SAIM  ARDO, CALIFORNIA

KERR-MCGEE CHEMICAL CORP.
TRUNAr  CALIFORNIA

QUALITY  MILLS. TNC.
,-lT.  AlHY, ,\'(JKTh CAROLINA

ttUNRt.  INC.
CA1KU,  iLLlMlIb

 TEXACO  IwCORPOKATEO
SAh  AROO, CALIFORNIA

UENF.hAL N:U10KS COHf'ORATIUN
UAYTUN,  OHIO

 ALYFSKA PIPELINE  SERVICE  CO.
 VALDEZr  ALASKA

 ARCO/PDLYMt RS,  INC.
 MONACA,  PENNSYLVANIA

 LA.XlluN  TEX1 ILES
 CANTUN,  bEORbIA

 CA1FKPILLAR  TRACTOR  CO.
 tAST PtURlA,  ILLINOIS

 CATERPILLAR  TRACTOR  CO.
 MAPLtTUN,  ILLINOIS

 CATERPILLAR  TRACTOR  CO.
 N'OSSVILLE,  ILLINUIS

 FlKFSTuNt  TIRE  Ai\i[)  RUHBER CO.
 POITSTUWN.  PENNSYLVANIA
CONTROL SYSTEM  PROCESS


SODIUM HYDROXIDE  SCRUBBING


CAUSTIC -vASTE  STREAM


CAUSITC rtASTE  STREAM


SOOIUM HYDROXIDE  SCRUBBING


SODIUM HYDROXIDE  SCRUBBING


CAUSTIC SCRUBBING


CAUSTIC SCRUBBING


DOUBLE ALKALI  (.DILUTE)


CITRATE PRuCESS


LIME  SCRUBBING


SODIUM HYDROxlUE SCRUBBING


       CARBONATE SCRUBBING
 WATER  SCRUBBING

 LIME  SCRUBBING

 SODIUM CARBONATE SCRUBBING

 SODIUM HYOROXIDE SCRUBBING

 SODIUM HYOROXIDF SCRUBBING

 DOUBLE ALKALI  CCONCEN T K ATED)

 CAUSTIC- WASTE  STREAM

 DOUBLE ALKALI  (.CONCENTRATED)

 DOUBLE ALKALI  (CONCENTRATED)

 DOUBLE ALKALI  (CONCENTRATED)

 DOUBLE ALKALI  (CONCENTRATED)
                                                 13

-------
                                                                                    STATUS AS OF U7/io/7a
                                       SECTION   4 (CONTINUED)

                         SUMMARY RY  VENDOR  OF  FGu  SYSTEMS UN IM)USIR1AL BOILERS
  VENDOR
  FMC  ENVIRONMENTAL EQUIPMENT
 GM ENVIRONMENTAL


 GREAI WESTERN SUGAR
 HEATtW  TECHNOLOGY


 KOCH FIMGINEEKING
MOttTL UIL COMPANY
    SELECTED
                                       INSTALLATION  MAMt  /  LOCA1IUN
                                      FMC  (SODA  ASH  PLANT)
                                      GREEN klVEk, WYOMING

                                      GENERAL hOTOHS  CORPORATION
                                      TONOnAftiDA, Nth  YORft

                                      GE 1 TY uIL  COMPANY
                                      BAKERSF icLo, CALIFORNIA

                                      1RANSCU TEXTILES,  IMC.
                                      AUbUSTA,  GEORGIA
         MOTORS  CORPORATIuM
 PAHMA, OHIO

 GRtAl WESTERN SUbAk
 rtlLLINbS, MONTANA

 GRtA f rtESTtrffM JiUGAK
 FIMDLAY, OrilU

 GREAI WESTERN SLIGAk
 KJKT MORGAN, COLORADO

 GREAI wESTfcRN SUGAk
 FRtEM()NT,()HIO
                                      URtAT
                                      GEklNG,
 GREAT  WESTtRN SUGAR
 bRtELEY,  COLORADO

 bRtAT  nESTEKN SUGAR
 LONGHOMT,  COLORADO

 GREAT  AESTtRN SUGAR
 LOvtLAivD,  COLORADO

 GREAT  ftESTtRiM SUbAk
 SCOTTS  HLUI-F, NEBRASKA

 MOtfTL  UIL  COMPANY
 bUTTUNwlLLOrt, CALIFORNIA

 ARMCU  STtEL
 HIDOLEIOwN,  OHIO

 CHtVRON U.S.A.  INC.
 BAKERSF IELL),  CALIFURUTA

 MIIMN-OAK FARMER'S COOPERATIVE
 rtAHPtTON,  iMORTh DAKOTA
PEAHUDY ENGINEERING
      uIL COMPANY
SAN ARDO, CALIFORNIA

C.A.h.(CARmuF-AMOCO-MUNSANTU)
ttnUSTON, TtXAS

CHtVtRljN U.S.A.  INC.
riAKE'RSFltLD, CALIFORNIA

bRISSOi'l Alk MlkCE HASE
HUNKER HILL, INDIANA

GENERAL hOIOKS CORKURATIUM
KINTIAC, MICHIGAN
  CONTROL SYSTtM PROCESS


  SODIUM  CARBONATE SCRUBBING


  SDDIIJW  HYDROXIDE SCRUBBING


  SOUIUI'  CAkitONATE SCRUHblNR


  soDiut--  CARBONATE SCRUHHING


  DOURLE  ALKALI  (DILUTE)


  AMMONIA-LADEN  PROCESS  WATER


 SODIU^ CARBiJNAIE  SCRUBBING


 AMMOiJIA-LADEni  PROCESS  rtAlER


 SODIUK CARdOiMAlE  SCRUBBING


 AMMONTA-LADEN PROCESS WATER


 AMMONIA-LADEN PROCESS WATER


 AMMONIA-LADEN PROCESS WATER


 AMMONIA-LADEN PROCESS WATER


 AMMdmlA-LADEN PROCESS WATER


 SODIUM CARoUHAiE  SCRURBING


 LIME SCRUBBING


 SODIUM CARBONATE  SCRUBBING


 AMMONTA  SCRUbHINb


 SODIUM HYDROXIDE  SCRUBBING


NOT SELECTED


SODIUM CARBONATE  SCRUBBING


DOUBLF  ALKALI (CONCENTRATED)


SO.DIU"1  HYOKllXlDE  SCRUBBING

-------
                                                                                         SIATUS  Ab  UF Il7/i-'ljHI3IiMG
CAUS I IC-rt4b ft


IVAIF.K  3Ct*UHrtING  CNAriMHi
    U!»  HYOKUXIDE

        ALKALI  (DILUTE)

DOUBLE  ALKALI  (DILUTE)

-------
                                                                                     STATUS A3 OF 07/30/78
                               OPERATIONAL  t-Ko  ;>Y;jlt.N!, DM INDUSTRIAL BOILERS
 ("U"HA;.!Y/L
    Mb-.*/
   tTKUFT T
UNIT !UZL
 (SCI M)
                                                                    PRUCESb/VFNDuR
START-UP
  MO/YR
 ALYtSKA PIPELINE  bERVICE CO.
 VALUE/, ALASKA
 FUF|_ UTL  (O.Oi*. -  O.U  SULFUR)
 N R ft
                  bO,000
                            SODIUM HYDROXIDE SCRUBBING
                            EMC ENVIRONMENTAL EQUIPMENT
                                              6/77
 AMfxTLAN  THREAD  CU.               RETROFIT
 '•iAKiOu, NORTH  CAROLINA
 CbAL  Id.8i  SULFUR);  INTERRUPT1BLE NATURAL GAS
                  1 fl , 5 0 0
                            CAUSriC-.«ASTt" STREAM
                            n.r,. SLY MANUFACTURING cu.
                                              0/73
 AKMCC STE-EL
 MlDi)LbTOWNf OHIu
 CUAu (0.8Z SUL^UR)
 HETRuFIT
                  84,000
                            LIME SCRUBBING
                            KOCH ENGINEERING
                                              0/75
 CANTON TEXTILES                   RETROFIT
 CAiVniiW GEORGIA
 CoAL ((1.8* SULFUR);  INTERRUPTI8LE NATURAL GAS
                 d5,000
                            CAUSTIC- WASTE STREAM
                            FMC  ENVIRONMENTAL EQUIPMENT
                                              6/77, 000
                           DOUBLE  ALKALI  (DILUTE)
                           ZURN  INDUSTRIES
                                              9/7 MISSOURI
CuAL (}.?.'/. SllLFuR)
WETROFIT
                 64,000
                           SODIUM HYIlRnxiDE SCRUBBING
                           A.u.  LITTLE
                                             o/^^
.JcNtRAL MuTORb CORPORATION
'ihY[(ii\i, OHIO
C..iAL(il.7X - a.Oz  SULFUR)
RFIRUFIT
                 36,000
                           SODIUM HYOkOXIUE SCRUBBING,
                           tNIOLFTER,  i«C.
                                             9/74

-------
                                                                                   STATUS AS OF  07/30/78
                                      SS-CT10N  5 (CONTINUED)

                              OPERATIONAL FGO SYSTtr"b UN  I.NfHISFRlAL  BOILERS
                                   RfcTKflF IT
                                                UNIT SI7E
                                                  (SCFM)
                                                                   PROCESS/VENDOR
                                                                                            START-UP
                                                                                              MO/YR
KEMERAL MOTORS CORPORATION
Tli''iu.-.A")UA, Nf.ft YORK
Cl'AL 11.2X SULFUR)
                                  REIRUFIT
                                                  V2.000     SOUIUM HYUROXIDE SCRUBBING        b/75
                                                             FMC  ENVIRONMENTAL EQUIt-MENT
fefltl'AL MUTORS CORPORATION        RETROFIT
PARMA, OHIO
CUAL  li?.5X SULFUR*  1.1%  ASH*  13,3bO Rlll/Lb)
                                                   128,aoo    DOUBLE ALKALI tnuuTt)
                                                             liM fc.MVIKJNMENTAL
        MOTORS CORPORATION
Pli"l T AC, MICHIGAN
CI,AL ift.84% SULFUR)
     .SHOD, PAPER,  AN!)  CARDBOARD.
                                                   107,iOO    SOUIUM HYDROXIDE SCRUBBING
                                                             PEABOOY
                                                                                               4/7b
GcOKBlA-PACIFIC  PAPtR  CU.         N£«Y
CtOISSfcTT, ARKANSAS
^^Arf^ AND OIL  OR  COAL  (1% - 1.5X SOLFOR)
                                                   
-------
                                                                                    STATUS AS OF (I7/JO/7H
                                       SECTION  5 (CONTINUED)

                               OPERATIONAL FGD SYSTtMb UN INDUSTRIAL  BOILERS
 COMPANY/LOCATION/FUEL
 ITT RAYUNIER,  INC.
 FERNANDINA BEACH, FLORIOA
 8ARK AND OIL  (2X - d.b%  SULFUR)
                                     NEW/
                                   RETROFIT
                                  Rt TKUFIT
DMT SIZE
 (SCFMJ
                                                                   PROCESS/VENDOR
                                                  t?01,uOC   SODIUM  HYDROXIDE  SCRUBBING
                                                            AIRPGL  INDUSTRIES
bTARI-UH
  NO/Yh
                                              O/
 KERR-MCGEE CHEMICAL CORP.         N
 TKOlMA, CALIFORNIA
 COKE, COAL, OIL  (O.bX - 5%  SULFUR)
                                                  7?b,OOU   SODIUM  CARBONATE  SC^UhBIIVG       b/7»
                                                            COwBUSTIUN  Eul)lHHF.,NiT  ASSuC.
 MtA.U PAPERBUARO Cu.
 STFVEIMSON, ALAHAMA
 OIL tl.5% - 31 SULFUR)
                                  Nfcrt
                                                  100,000   SODIUM HYDROXIDE  SCKUbblMG       0/7b
                                                            AlKPOL INDUSTRIES
MINN-DAK FARMER'S COOPERATIVE
WAHPElOiM, NORTH DAKuTA
LIGNITE  Cl.OX SULFUR)
                                  RETROFIT
                                                   160,000   AMMONIA SCRUBRINr,
                                                             KOCH ENGINEERING
                                              b/77
 MUH1L  OIL COMPANY
 SAN  Awr>0, CALIFORNIA
 OIL  Id.OX - 2.P5X SULFUR)
                                  RETROFIT
                                                            SODIUM HrnRoxiuE SCRUBBING        0/74
                                                            MOolL UIL COMPANY
 NEKUOSA  PAPERS,  INC.
 ASHUdAN,  ARKANSAS
 COAL  tix-i.sx  SULFUR)
                                 NErt
                                                  •ill,000    CAUSTIC SCRUBBING
                                                                   INDUSTRIES
 RICKENHACKFR  AIR FORCE BASE
 COLUMBUS,  OHIO
 COAL  (i.M  SULFUR)
                                 RETROFIT         50,000     LIMESTONE SCRUBBING
                                                            KESEARCH-COTTRELL/dAHCU
                                             3/7b
SHEuLtR  GLOBE  CORP.
NORFOLK,  VIRGINIA
COAL  ILESS  THAN  IX  SULFURJ
                                 RF1RUFIT         B,000      SOuIUM  HYDROXIDE SCRUBBING
                                                            W.rt.  SLY  MANUFACTURING CO.
SI. REGIS PAPER  Cu.               RETROFIT
CANTOIMMENT, FLORIOA
BARK AND GAS OR  OIL  (LESS^HAN  IX SOLFLIR)
                                                 115,000   CAUSTIC  SCROBBIMb
                                                           AIHPOL  INDOSIRIES
                                             0/7i
TEXACO INCORPORATED
SAN ARHO, CALIFORNIA
OIL (1.7X SULFUR)
                                 RE TRUFIT
                                                 366,000   souiuM  HYDROXIDE  SCRUBBING
                                                           CE1LCOTE
TtXASGIJLF
GRANGER, WYOMING
UIL (1.1X SULFUR)
                                                 I«0,o0u   SODIUM CARbONAIE  SCRUBBING        q/7b
                                                                  INC.
                                               1H

-------
                                                                                  STATUS Ab OF 07/30/7(1
                                            SF.U If)hi   h

                               CONSTRUCTION  FuO  SVSTtMS  Oi\ 1NDUSTKIAL HOILFkh
COMPANY/LOCATJON/FOtl
                                     Mt«/
                                   ETwOFIT
                                                UNIT  SIZt
                                          lAKT-UP
                                           Ml/Yk
CATEkPTLLAW IrtACTOR Co.
^APLF.ION, ILLINUIS
CuAu (3.2% SULFUR)
                                                  1-57,000   IJOUBLE ALKALI lCo^CFf^.^Kf» IEO)     10/7B
GtTFY OIL COMPANY
BAKERSFIELD, CALIFOkNIA
CRUDE OIL (1.1X SULFUR)
                                  Kt IRUFIT
993,750   SODIUM CARBONATE
          PRuPRIATARY OE81UN
                                                                                             12/7b
GREAT WESTERN SUGAR
FrtEfcMONT.OHIQ
COAL C3X SULFUR)
                                  RETROFIT
                                                  4 0 , 0 0 0
          SODIUM CARBONATE  SCRUBblNG
          bR£AT WESTERN  SUGAR
                                                                                             10/7b
MOBIL OIL COMPANY
BuTTONWILLOn, CALIFORNIA
OIL d.ix SULFUR)
                                  RETROFIT
                                                    ,000
          SOuIUM CARBONATE  SCRUBBING
          HEATER TECHNOLOGY
                                                                                              9/78
ST. JOE ZINC CO.
MONACA, PENNSYLVANIA
COAL  U.5X-4.SX SULFUR)
                                  RETROFIT
10<4,00u   CITRATE PROCESS
          bUREAU OF MINES
                                                                                             10/7S
TEXACO INCORPORATED
SAN ARDO, CALIFORNIA
U1L (1.7X SULFUR)
                                  RETROFIT
117,000   SODIUM CARBONATE  SCRUBBING
          DUCQN COMPANY
                                                                                              3/79

-------
                                                                                    STATUS AS OF 07/40/78
                                             SFuTiOiM  7

                                         K;U  hYbTfb uN InHuSFRlAL dOILERS
                                          1 I
                                                 ' M T S 1 7 E
                                                                   PROCESS/VENDOR
                                                          START-UP
                                                            Ml/YR
Awro/POLYMERS,  INC.
^uNACA,  PENNSYLVANIA
CuAL  tl.O/S  SULFURJ
KETRQFIT
                           uouaLE ALKALI  (CUIVCENTRATEU)
                           FMC tNVlKUNMENTAL  tQUIPMENl
 6/80
CARtUlKUNPUM  AtiRASIVtS            KFTRUFIT
rtuFFAL'l,  ,MEW  YORK
CL)AL  UX  S AVERAGE,  3.8« S DESIGN MAX)
                 3fi,000
                           LIMF SCRUBBING
                           CARriORUMDUM ENVIR.  SYS.  LTD.
 O/ 0
CiiEVFRON  U.S.A.  INC.
rtAKfcWSFIELO,  CALIFORNIA
OIL (1.1%  SULFUR)
KETRUF1T
                 116,000   SODIOM CAR80NAIE SCR08SING       1/79
                           NOT SELECTED
      M AIR FORCE  BASE
tiUNKhn HILL,  IiMDIANA
CiiAL (0.9* -  4.fa)C  SULFIIrt)
1 NE« £ KETRuFiTia,000
                           DOUBLE ALKALI  (CONCENTRATED)
                           MOT SELECTED
 9/79
C.A.M.lCAKBIOE-AMUCG-MOiMSANTO)
HOUSTON, TEXAS
MuT SELECTED
NEW
                 l,dOO,000  NOT  SELECTED
                           IMO]  SELECTED
10/83

-------
                                                                                  STATUS AS OF  07/30/78

                                           SECTION  R

                          Oh  inSPuSAl.  PRACTICES FJR FGP SYSTF-.HS  0,M INUUSTklAl  BOILERS
INSTALLATION NAMt  / LOCATION
                                     STATUS/CuMMElvTS
Al.,\ALliME SULHTt/msoLU ie  KtCYCUtl) ID PULP PHUCtSS
i.lFAl) PAPEHbOARD CO.
&TF-VHNSOiMi ALABAMA
        PAPERS,  INC.
ASnr>i>''M, ARKANSAS
OPERATIONAL
RECOVERED SOLUTION  USED  AS  MAKE-UP TO COOKING LIUUOR  IN  PULP
MILL.

OPERATIONAL
SDiJ KE'COvEn'F.D HP.OM  SUOIUh SDLFITE/SULF ATE LIQUOR  AND  RE-
LYCLtD TU PULPING PKJCESS.
          SLURWY  Tu  LANDFILL
AKCd/PJLYMERS,  INC.
        PENNSYLVANIA
bUNGE, INC.
      , ILLINOIS
t.» IfKPiLLAM  TRACTOK  CO.
tAbT PtOi«IA,  ILLINOIS

CATcnPILLAK  TWACTOK  CO.
i-ilJSSV ILLtf  ILLINOIS

CAIEKPILLAR  FRACFOK  CO.
JOLlcT,  ILLINOIS

CATI-NPILLAK  TRACTOR  CO.
MOKTUN,  ILLINOIS

CAIFHPtLLAR  TRACTUK  CO.
("APLclON,  ILLINOIS
           TIRE  AND RUBHEH CO.
HOiTaTowi\i,  PENNSYLVANIA

uf.iMEKAL MOTORS  CORPORATION
            NtW'  YORn
CiFiMKKAL MOTORS  CURPOKATIUN
t'Ai,^A, OnIO
        MOTORS  CORPORATION
KO«TIAC»  MICrilbAlM
         AIR  FORCt b«SE
        HJLL»
U.S.  (iYPSUH  CO«P.
PLANNED-CONTRACT  AWARDED
FLYASH AUDITION  TO  OEWATERtn CAS03/CASUa FILTER  CAKF.,
THEN TU LANDhILL.

TERMINATED
OPERATIONAL
60+% SUL1DS  CCASoa)  SLUOUE DIRECTLY TO LANDFILL

OPERATIONAL
bO + X SOLIDS  CCASU«)  SLUOb'E DIRECTLY TO LANDFILL

OPERATIONAL


OPERATIONAL
CONSTRUCT ION
bO+% SOLIDS  ICASO
-------
                                                                                    STATUS AS OF 0//3U/7B

                                       SECTION  8 (CONTINUED)


                    SUMMARY  OF  DISPOSAL PRACTICES FOR FGD SYSTEMS ON  INDUSTRTAL  BOILERS




  INSTALLATION NAME / LOCATION        STATOS/COMKENTS



  HOLDING POiMD FOR  EvAPOxAIIuN                     "      		




  ^i""?* ASH..^A?T1                 OPERATIONAL
                                                  !;»"»«  «»>«•« TO COLLECT PUND - NO PRIOR
                                                  LANDFILL  IN THE FUTURE
  GETTY OIL COMPANY                   OPERATIONAL
                                      10 GPM  BLEEDOFH  TO  A  BLO^U^N , ANK .   THE BL0«OO.N  IS  THEN
                                           TO  A .DISPOSAL  PUNu  ONCE A WEEK.

  KEKR-MCG.EE CHEMICAL COWP.           OPtRATlOivAL

         CALIFORNXA                   «KUHB« EFFLUEN, IS  CLAKtFItO ANO THE, PUT INTO A MINERAL



                                      UP.RATZONAL



        OIL  COMPANY                   CONS1PHC1 ION

                                      INlERMiHE.T B.LO.DONN  TO  ,ASTE DISPOSAL S!rE.



 NOIM-FIXATEU  SLURRY  To  LINED  POM)                                          " ----- " ----------------




 CANTON TEXTILES                      OPERATIONAL

 CANTON, GEORGIA                      WA  SU3/SU LIQUOR UISPOStD TO  LINED  HOLDING PONDS


 RICKENUACKER AIR  FuRCE  BASE          OPERATIONAL

 COLUMrtUS, O.HIO                       UNSTA8IL1ZEO C»Sy3/SU/l SLOuGE  TO LINED  POND



 KEbENEHABLE - ELEMENTAL SULFOR  PKOUUCT            "         ""'                 " ------------------



 ST. JOE ZINC CO.

 MJNACA, PENNSYLVANIA




 (VASTEWATER TREATMENT AND IHSCHARtt To CITy'sEWEH
         MOTORS CORPORATION          OPERATIONAL


 ST.  LOOIS,  MISSOURI                '???y"L°X '°!ZEl)  '°  NA2bt"*'  PH  ^^TRALIZED AW DISCHARGED TO
                                     LI IT bfcWhW SYSfFNi
GENFKAL  MOTORS  .COHPOSATION


                                                          3, GP,  ,0  ON-SirE  CLARIFICA T ION AND
GEORGIATPACIFI.C  PAPER  go.            OPEWATIOMAL
CRuSSETT,
GREAI WESTERN SUGAR                  OPERATIONAL

FINDLAY, OHIO                        bLEED-OFI- STREAM TO HOLDING  TANK


CHEAT WESTtRN SUGAR                  CONSIRUCHUN
Fh'tFMONT.OHIO


UMAL1FY MILLS, INC.                  TERMINATED

MT. AIRY, NORTH CAROLINA             SCABBING LIUHUR DISCHARGED TO Nt U F R AL I I AT 1 1)>4  POND

-------
                                                                                 STATUS AS UF 07/.50/7B
                                    SECT ION  8  (CO.  ! if-uMj]

                 SUMMARY OF DISPOSAL HnALTJCKS FUK  FI;|I SYSTEMS
                                                                   I \ijlJSTK I Al  tt.JILEl™»»«™™^™»" — •» — — ™"~™™™~'"~~~~ — "~~~"


                                     OPERATIONAL



                                     CONSTRUCTION
CHEVRON U.S.A. INC.
tiAKERSFIELDr CALIFORNIA
GETTY OIL COMPANY
bAKERSFIELO, CALIFORNIA

ITT KAYONIEW,  INC.
FERNANDINA BEACH, FLORIDA
                                     OPERATIONAL
WASTEWATER TREATMENT
ALYESKA PIPELINE  SERVICE  CO.
VALDE/, ALASKA
CHEVERON  U.S.A.  INC.
BAHERSFIELD,  CALIFORNIA
MINN-DAK  FARMER'S  COOPERATIVE
HAhPETON,  NORTH  DAKOTA
ST.  REGIS PAPER  CO.
CANTONMENT,  FLORIDA
 TEXACO  INCORPORAIEU
SAN  ARUO,  CALIFORNIA
                                     OPERATIONAL
                                     iMASSU3/HSOi AF.kATEU TO NAi2S01 AND  TRANSFERRED  TO  WASTEWATER
                                     TREATMENT  PLANT AT A RATt UF lu GPM.   IT  13  MIXED WITH  ABOUT
                                     10,000  GHM OF  BALLAST HAIEK FROM TANKERS  IN  HOnT  VALDEi.
                                     CLEANED ft'AIEK  IS TMEln OlbCHAreGEO IwTO  PORT  VALuEZ.

                                                     IMG/EVALUATING BIDS
 TEXAbGULF
                                     OPERATIONAL
                                     BLEED STKEAM GUES TO AN ACTIVATF-D  SLUDGE  SYSTEM  a  lb(J GPM

                                     OPERATIONAL
                                     EFFLUENT IS TREAIFU IN Aw uN-SlTt  SEmAGF  TREATMENT PLANT

                                     OPERATIONAL
                                     HALF OF IHt SCRUdBER UNDERFLOW  IS  TREAIFU AND  RECYCLED AS
                                     BOILER FEEuWATtR; THE uTrIEK nALF GOFS  10  WASTEwATEK
                                     l/ISPOSAL wtl LS.

                                     OPERATIONAL
          WYOMING

-------
                                             STATUS AS OF


SFlTJOiM  a  (CUrjTllvuFOl




                                          HUILEKS
                  SUMMARY OF OISHOSAL  HKAUTICtS FOR F«D S, STEMS ON JNUUSTKIAL






 INSTALLATION NAME / LOCAIIuN        STATUS/COMMENTS




 uvtRFLuW  Tu StntR/SLiiDbt Tu LAfMDFlLL
         GLO«t  CORP.

NtlKFuLn.  VIRGINIA
UtaPOSAL  TtCHNIOuE NOT KNOnN
                                     HLANNFO-CONSZOtRlNU  802  CONTROL
HARRIS MINING  to.                    TERMINATED
SPRUCE PINE, NORTH  CAROLINA         itKMJNATEO
SCHIIoBER EFFLOENT  DISPOSED  OF  IN
IEXACO INCORHORATfO                  CONSTRUCTION

SAn ARUO, CALIFORNIA

-------
                                                                                   STATUS AS UF 07/JO/7H

                                            SECTION  9
                PERFORMANCE DESCRIPTION FOR uPtRftllONAL KGl)  SYSTtMS  ON ' IUPuS1R1AL BOILERS
  INSTALLATION NAME
  I'MSTALLAIIUN LOCATION
  SOul'Ct  CHARACTERISTICS
  SHIlkCF  HATING
  MJi-:titR  OF  SEPARATE FUO UNITS
  SOURCF  CAPACITY
  LOiMTtVOL SYSTEM VENDOR
  CO,\TRUL PROCESS
  wtn /  RETROFIT
  START-UP DATE
  CONTROL SYSTEM S1AIIIS
  Slid EFFICIENCY
  PAKTICULATfc EFFICIENCY
  AA1F.R  MAKE-UP
  SI.UDbF  OK BY-PRODUCT DISPOSAL
ALYEbKA PIPELINE SERVICE CO.
VALOEZ, ALASKA
t-ufcL OIL (u.ojx - u.i* SULFUR)
50,01/0 SCFIW   (DESIGN MAXIMUM)
 1
25 Mft  (FUUIVALENT)
FMC tNVIWONMENTAL EQUIPMENI
SOOlOM HYDKOXIUE
  CONTROL SYSTEM COST
JIIME, 1977
OPERATIONAL
<»6 + % (15U-160 PPM oi  INLET)
PAKT1CULATE EMISSIONS  MEET  NSPS.
10 GPM - OHEN LOOP
V.ASTEHATER TREATMENT
NAdSOi/HSOi AEKATEO  TO NA2S01  AND TRANSFERRED TO WASTEWATEk
fREAIMEN'l PLANI  AT A RATE  OF  lu  GPM.   IT IS MIXEO rtlTH ABOUT
10,000 GPM OF bALLASl  rtATER FROM  TANKERS IN PORT VALDEZ.
CLEANED HATER IS THEN  'OISCHAKGtD  INTO PORT VALOEZ.
LAPIIAL: PLANT PERSONNEL  no NOT  HHEAK our FGU SYSTEM COSTS
     OVERALL PiPtLiNt  PROJECI
                                                    :  PLANT ALCOUNTING OOES NOT KEEP OPERATING COSTS
                                           FUR  THE  INERT  GAS (FGD)  SYSTEM.
                                       bACKGKUOND  INFORMAIION
     AI THE VALOEZ TERMINAL OF  THE  ALASKAN  OIL  PIPELINE,  ALYESKA PIPELINE SERVICE COMPANY OPERATES
IHt OIL STORAGE AND TRANSFER FACILITY.   OIL FLOWING IN FROM THE PIPELINE IS  (EMPuRARILY STORED  IN
BE\/FKAL HUGE TANKS, THEN TRANSFERRED  FROM  int  TANKS TO OIL TANKER SHIPS IN NEARBY PORT VALOEZ.
ALYEbkA i\iEtOtD NEUTRAL BLANKET  AIR  FOR  THE  OIL  SIORAbE TANKS,  A LOW OXYGEN CONTENT BEING PARTICULAR-
LY ntSlRABLE.  II WAS UEfExMlNED  THAT  UN-SITE  bOILER FLOE GAS  nOJLO HAVE THE REUUIWED LOW OXYGEN
co«TtM .  CORROSION PREVENTION  IN  THE  OIL  STORAGE  TANKS OICTATED THE NEED FOR sod CONTROLS.
THAT IS, THE DEVICE WAS NOT INSTALLED  TO MEET  AN  EMISSIONS REGOLATION.  NEVERTHELESS, THE
"Uif'KT I^AS" SYSTEM IS BASICALLY A  SOOIOM HYDROXIDE  FGD SYSTEM  AMO WAS DESIGNED AND INSTALLED BY
h"C rJWVTRONMENT AL EQUTPMENT OIVTSIUN.
     Tut BOILERS DO NOT OPERATE AT  STEADY  STATE  CONDITIONS. THIS IS OUE TO THE FACT THAT WHEN OIL
IS RE"ui/tI) FROM Tht TANKS AT A  FASTER  RATE  THAN  IT  IS bFiNG FED ttY THE PIPELINE, AN ADDITIONAL  INERT

-------
                                                                                     STATUS AS OF 07/.50/78
                                        SECTION  9  (CONTINUED)
                  PERFORMANCE DESCRIPTION FOR OPERATIONAL KC-D SYSTEMS  ON  INDUSTRIAL  bORERS
  ALYESKA PIPELINE SERVICE CU.; VALDtZ, ALASKA (CONTINUED)

  AIR BLANKET IS NEEDED. THIS REuOIRES INCREASING ,Ht UOILtR LUAU FROM  THE NORMAL LEVEL  OF  PLANT
  PO-ER PRODUCTION TO RUN THE COMPRESSORS AND PRODUCE ADDHIONAL GAS FOR BLANKET PRODUCTION.
  if  THE TANKS ARE FILLING EASIER THAN THEY  ARE BEING EMPTIED, THE AI.  FORCED OUT br  THE  INCOMING
  OIL WILL  BE INCINERATED.

       THE  BOILER  PLANT  AT THE VALUE* TERMJNAL CONSISTS OF THREE 250 MM BTU/HR OIL-FIRED  BOILERS,
  MANUFACTURED BY  COM8US,ION-FNG,NEERING.   THE OIL  BEING USED IN ,hE BOILERS PRODUCES A  VERY  LOW
  PARTICULATE GRAIN  LOADING.  AN0  HAS  A, EXTREMELY LOW SOLFOR CONTENT WHICH RANGES FROM 0.0«  TO  O.U.
  THERE  .IS  NO PAKTICULATt  CONTROL  OTHER IHAN  WHA,  OCCURS I,  THt  H,C SO, ABSORBER MODULE.
       THE  MAXIMUM DESIGN  CAPACITY  OF  THE  SCRUBBER  MODULE  IS 50,000 SCFM,  *HICH REPRESENTS  ABOUT 2S»
  UF  THE  TOTAL  FLUE  GAS  GENEHAIED.  THE 50i CONTKOL  SYSTEM Is DESTINED ,£TH 10o% REDUNDANCY,  I.E.,
  fHEPE  ARE TWO  MODULES  IN PARALLEL,  ONLY  ONE  uF  WHICH  IS  IN USE  AT  ANYTIME.
      CAUSTIC  (SODIUM HYDROXIDE,  IS  USEO  AS  REAGENT MAKE-UP. DESIGN PH CONTROL WAS AHOUT 6.5, BUT
 OPERATIONS  HAVE  INUICA,Eu  ,HAT A  HIGHEK  PH  IS ,0,E DESIRABLE,  ,0  CON,KOL PH IS NO, AttOoT 8.0.
 A BLtEU STREAM OF SOD.OM 8ISOLFITE/SOLFI,F  GOES TO AN  AERATOR  AT  A  RATE  OF  ,0  GPH.   AF.ER COMPLETE
 OXIDATION TO NAB504.. TnE WASTE STREAM GOES  To A hASTthATtR  TKEATMENT  AHEA «HtRE  IT  IS  MlXEu .IIH
 10,000 GPM OF BALLAST «A>EK FROM  THF  TANKERS  I,, , HE PORT,  AND DISCHARGED  INTO  THE  PORT.


                                         OPERATING  HISTORY
 3RD  UUARTEK-I977     CORROSION HAS OCCURRED IN 'I HE  PIPING FOR THE WATER RECIRCULAT ION SYSTEM.
 AT THE TIMt  OF THIS REPORT, ,HE CAUSE «A3 NOT KNOWN.   ALYESKA TESTS HAVE  DEMONSTRATED  ABOUr
 5 PPM S0d/803/80a AT THE ABSOfiuFri OUTLET.  INLET Su2 CONCENTRATION  RANGES FHOM ISO  Tj  160  PPM.
 THE  SYSTEM WAS THEREFORE REMOVING ABOUT 96%  OF THF  INLET SoLFUR OXIDES.   AT THE  ,IME OF  THIS REPORT,
 THfRE WAS  NO CONIINOOOS bO«e MONITOR  ON THE  SYSTEM.

 «TH  UUAR1EH-1-177      THE CONTROL SYS,EM OPERATED NEARLY PRUBLEM-FREE,  WITH NO DOWNTIME
 BEING ASSIGNED TO THE  SO* REMOVAL SYSTEM.  THE CURRENT LOAD IS  APPHOXIMAIELY ->U* OF  DESIGN
 CAPACITY.  THIS IS  A RhSULT OF OIL FLO» BEING LO.AT PRESENT.  PLANS ,£RE *ti^ MAOE To  DEAL  WITH
 THE  WET  AREAS CORROSION PRORLEM  HY TlJ TKODIIC ING NEUTRALIZING AMINE SPRAYS.


 1.ST  UUARTEK-1978     DURING  THIS  PERIOD,  THE  CORROSION  PROBLEM WAS ALLEVIATED RY SPRAYING HYDRAZINF
 !NTO  THE SYSTEM UPSTREAM .OF  THE  MIST  ELIMINATOR.   ,'HIS  MEASORE  RAISED FRoM 4 TO b.S  THt  PH OF tHE
LIUUOR  RECOVERED  BY  I HE  MIST  ELIMINATOR.  CYCLoHEXAMJNt MAY  bE  TESTED iN  PLACF  OF  THE HYORAZlNE.
THE PLANT  WAS  NOT YET AWARE  UF THE CAUSE  OF  THE  CORROSION,  ALTHOUGH .H£Y  SOSPFCTtD CARBON, SULFUR,
AMD NITROGEN  ACID GASES.  CHLORIDES  HAVE  VIRTUALLY  BEEN RULED OUT  AS THE  SOURCE OF THE  CuRKOSION.


^ U..AR,EH-m«     .Ht FMC FGD SYSTEM CUMUNUED TO OPERATE  ON  A  CONTINUOUS  HASIS,  BEING RfSPONSl-
BLfc l-nn NO DOWNTIME.  ANY MAIN.ENANCE  OPERATIONS ,ERE tFFECTED WHILE  THE  SYSTFM ,vAS  OPERATIC.

-------
                                                                                   STATUS A3 UF U?/iO/76

                                      bFCUOiv  4 (COhiT INJEij)
                PERFUNMANCE  uEbCRIt-THJN KUK OPt XA I lO.'i AL HIS,)  .YSTtMa  UN  I ivOUS T-< 1 AL HlULtMS
  INSTALLATION  NAMt
  INSTALLATION  LOCATION
  SOURCt  CMARACTtRISI KS
  SOURCE  RATING
  NUMBER  Oh  SEPARATE FGD UNITS
  SQUhCE  CAPACITY
AMtKlCAN T H rt t 4 i) CO.
MAKlUN, i\lOhTH CAROLINA
LOAL (O.rtX SULFUR);  INT KrtHUPT I&LF-  inATUKAL i.AS
i«,5oo SI:FN CTUTAL - 2 HUTLFKS)
   Mft (EuUlVALtM); TOTAL  -  ^
 CONTROL  SYSTtM  VtNOUK
 COivTxOL  PROCtSS
 NEW  /  HEIRUFJT
 bTART-UP UATt
 CONTROL  SYSTEM  STATUS
 SOi  EFFICIENCY
 PAKTICULATt EFFICIENCY
 SLUObF. OR iJY-PWODlJCT DISPOSAL
n.tt. SLY MANuFACrilKluG CU.
CAuST IC-WA6Tt aTKEAM
KE IRUFIT
197 J
UPtRATlONAL
1QX.
  CONTROL SYSTEM COST
HOLDING POMO  FOR  EVAPOKATION
THE SOUIUM  SULFITE/SULFAfE WASTE LIQUOR IS PUMPED  TO
A KEU CLAY  LINtO  ASH  8ASI>M.   LEACHING OF THE SOLUBLE  SODIUM
SALTS IS THEKtiiY  PREVENTEO.
CAPITAL: $i3«,ooo tis/a).   THIS is TOTAL INSTALLED COST.
                                           OPtRATINt.:  $lh,?00/Yk 11977).  THIS FlbUftE  iNCLUuES  i
                                           FlbEKGLAiS  LININGS IN UUCTwORK AND ON FAi\iS  Awl)  OIHER
                                           OPERATING LABOR AND MATERIALS.
                                          OPERAIING HISTORY
    PLANT KEPOHTS THAT IT  IS STILL  EXPERIENCING SChUbBtR 1.0. KAN PROBLEMS  HUE  Tu  VloRATIOiM AND
CORROSION.  TO OVERCOME  THIS PHOriLEM,  PLANS ARE HE1NG MADE TO ELIMINATE  THE  1.0. FANS  ON  THE
SCRUBBER AND UPGRADE bUlLEH  ID  FANS.
    OTHER PROBLEMS HAVt  flEtN AS FOLLOWS:
      1. VIBRATION CKACKb  IN PVC PIPING.
      2. FAILURE OF PUMP RUBBER LINING.
      1. THE NEED TO ORAIN THE  RtClWCULAHuN TANK AMU PAINT  IT WITH tPOXr  PAINT TO ALLEVIATE
         CORROSION PROULEMS.

-------
                                                                                     STATUS A3 OF 07/30/76



                                        SECTION  9  (CONTINUED)




                  PFRFURMA,,Ct  DESCRIPTION R)K OPERATIONAL F6,.) SYSTEMS  UM  INDUSTRIAL BOILERS
   INSTALLATION NAME




   INSTALLATION LUCATldm




   sooRuf CHARACTERISTICS




   SrtlJkCt RATING









   ullMRER OF SEPARATE FbD  UNITS




   COivTKOL SYSTEM VENDOR




   CONTROL PROCESS




   I'jF-tv / RETROFIT




   STARf-uP DATE




   CONTROL SYSTtM STATUS




   aOc> fcFKICItNCY




   SLuObE OK BY-PRODUCT DISPOSAL
ARMCU  STtEL.




i"lIOOLEIO«N,  UH10




COAL  Id.oZ SULFUR)




8i,ooo SCFM  (TOTAL  -  a  BOTLERSJ




dOO.OOO L8/HR STtAM (TOTAL)



 1




KOCH ENGINEERING




LIME SCRUBBING
19/b




OPERATIONAL




NOT AVAILABLE




hOLOINb POND FUR EVAPORATION
                                         BACKGROUND 1NFOKMATION




     THE SCRUBBER UNIT SERVES Two MULTI-RETuRT.  UNDERFEED STOKER, COAL-FIRED BOILERS,  EACH  *ITM A




 CAPACITY OF 100,000 LBS/HR STEAM.   THE  COAL  BURNtD  IS  TYPICALLY 0.7 TO 0.9 PERCENT  SULFUR




 AMD  d%  TO 10% ASH.  NORMALLY THE RulLERS  ARE  OPERATED  IN THE WINTER MONTHS ONLY, HOWEVER FOR  THE




 PAST  TWO YEARS,  uPERAT HNS HAVE BEEN  YtAR-ROUNU  WITH REDUCED CAPACITY DURING THE SUMMER.




 IHE  CONTROL SYSTtM CONSISTS OF A VARI AdLt-1 H«OAT  VEMIIRI SCRUBBER .(IfH A PRESSURE DROP CONTROLLED




 AUJUdTABLF  PLUG.  IMMEDIATELY uOwNaThEAM  FROM  I HE VENTuRI  IS An ABSORBER MODULE 17  FEET IN




 DlAMtTLR WITH THREE GAS SCRUBBING TRAYS,  A S-TYPt CHEVRON  MIST ELIMINATOR AND A 106-INCH DIAMETER




 STUB  STACK.   THE SYSTEM IS DESIGNED TO  HANDLE  1
-------
                                                                                    STATUS AS OF 07/iO/78





                                       SECTION  9 (CONTINUED)




                PF.RFURM*i\lCt UESCKTHTION  FOR  UPt« A T JON AL FGl) SYSTEMS ON  INDUSIRIAL  BOILERS




AHi-i;u STEEL; MIDllLtTlcMMf OHIO  ICuMT Iin
PIPT'.r; ]N ItUS SYSTEM rtAb  MTLO  STFtL  ANO HAS StVtRLY ABRADED CAUSING  NUMEROUS  LEAKS.




    1Ht SYSTEM HAS RtF.iM  1-iUOIFItD  Tu A uiMCt -T HRUUGH OPERATION AND  THE  ABRASION  HAS CEASED.




SHRIUHS ABRASION PRObLt^S  f,ERE  ALSO tNCOuNIEKEli IN 1,2-INCH STEEL  PIPING  CARRYING P1KTY WATER FROM




Irtt IWAY3 10 THE RECYCLE TANK  AS  rttLL AS IN IHt PUMPS.   THE PROBLEM  «AS  SOLVEH BY KEPLACINu THt




HlKl-jf- -ITH KUBBEH HUSfc,  RUR6EK LTIMtO ELBIMS,  ANO RUhHER LINED  POMPS.   IN ADDITION, PUMP SPEED WAS




KKiyllCfcU FROM 1780 TO  1180  KPM  AND FLANbEU T-SECTlOwS «bRE  INSTALLED  ON THE SUCTION SIDE OF THE




SLUIibE POMPS AND RtClRCULATION  PUMPS.  THIS MA1ERIAL HAS rtlTHSTHOI)  ABRASION HETTEK THAN ANY OTHER




,-iAIFKIAl. TRIED TO DAtF.



    A LIME BUILD OP PROBLEM WAS EXPECTED ON THt ABSORBER TRAYS  AT  LOW GAS FLOU RATES.  THIS




PROBLEM HAS NOT  YET OCCURRED A[ SUSTAINED PH LtVtLS OF h-6.5.



    THt LIME SLURRY SYSTEM HAS  ALSU PRESENTED A PROBLEM.   CLOGI.ING  OF THE LIME SLURRY LINE is




ATlRlnuTtD TO  ITS EXCESSIVE LENGTH.  LIME ADOHIuN RATt  IS A PROBLEM WHICH CAN BE RESOLVED WITH




IHt INSTALLATION OF A PROPORTIONAL LIME sLAKER.








                                          OPEKAIING HISTORY




4TH UiUARTER-l1)??      ThE PLANT WAS NOT  ABLE TO SUPPLY  EXIENSIVE OPOATE INFORMATION FOR THIS REPORT




HFkTui),  ALTHOUGH REPORTED IHAT RECENT OPERATIONS  HAVE  UFEN RELATIVELY PROBLEM-FREE.   THE SCRUBBER




rtAb DO. KM  IN FEBRUARY  1S7B AS A RESULT OF THE POWER SHORTAGE  OHIO IS EXPERIENCING.




PLANT  HAS  INDICATED  THAT II WILL SoPPLY MOnE DETAILED  INFORMATION FOR IHt ,MEXT REPORT




PF.KTuli.






dnu UUARTER-1978    IvO INFURMAIIUN flIAS  OBTAINED FOR  THIS UPDATE.

-------
                                                                                    STATUS AS OF 07/30/78



                                       SECTION  9  (CONTINUED)




                 PERFORMANCE DESCRIPTION FOR OPERATIONAL FGO SYSTEMS  UN  INDUSTRIAL BOILERS
   INSTALLATION NAME




   INSTALLATION LOCATION




   SOURCE CHARACTERISTICS




   SOURCE RATING




   NUMBER OF SEPARATE FGO UNITS




   SOURCE CAPACITY




   CONTROL SYSTEM VENDOR




   CONTROL PROCESS




   NEW  /  RETROFIT




   START-UP DATE




   CONTROL SYSTEM STATUS




   S02  EFFICIENCY




   PARTICULATE  EFFICIENCY




   rtAIER  MAKE-UP




   SLUDGE OR BY-PRODUCT  DISPOSAL









   CONTROL SYSTEM COST
CANTON  TtXIILES




CANTON, GEORGIA




COAL  (O.rtX  SULMIR);  IiMTERRUP T IBLE  .\iATURAL GAS



.55,000  SCFM  (1 BOILER)




 1




10 Mrt  (EQUIVALENT)




FMC tNvIRONMENTAL  EQUIPMENT




CAUSTIC- WASTE STREAM




RETROFIT




JUNE,  1974




OPERATIONAL




70* (500 PPM H INLET)




BOX - >>0% (5.9d L6/MM BTU  AT  INLET)




UPtN LOOP




NON-FIXATED SLURRY TU LINED POND




ivA S03/SU4 LIUUOR DldPOStn TO LINED  HOLDING  PONDS




CAPITAL COST IS FOR AM  INSTALLED SYSIEM.
                                        BACKGROUND INFORMATION




   CANTON  TEXTILE  MILLS  IN  CANTON,  GEORGIA HAS A 10 MW (EQUIVALENT) STEAM BOILER WHICH  FIRES  COAL




I-RUM OCT.  TO' MAY AND  INERUPTABLE  NATURAL GAS THE REMAINDER OK THE YEAR.  THE BOILER  IS  A  COMBUSTION




ENGINEERING  (C-E)  VERTICAL  UNIT  EQUIPPED WITH A CYCLUNIC RUST COLLECTOR.  THE DUST COLLECTOR




CAPTURES APPROXIMATELY 75  10  100  POUNDS UF FLY ASH PtR HOUR.  THE TYPICAL COAL BORNEO HAS  A SULFUR




CONTENT OF 0.8 PERCENT AND  AS  RECEIVED  HEAT  VALUE UF 13,faOO BTU PER POUND COAL.  SULFIlK DIOXIDE




CONCENTRATION IN FLOE GAS IS  1500  PPM WITH A PARTICIPATE LOAulNG UF 3.92 LB/MM BTU.




    THE HGU  SYSTEM CONSISTS UF A  FMC MEDIUM  ENERGY,  VENTURI-TYKE SCRUBoER.  CAUSTIC  DYEING WATER




WASTE CONTAINING SODIUM  HYDROXIDE  AND SOOIOM SULFATE WITH A PH OF APPROXIMATELY 11 To U  IS THE




SCRUBBING LIQUOR.  THF SCROBUING  LIQOlU IS INJECTED  INTO THE FLUE GAS STREAM THROOGH SPRAY NUZZLES




AHEAD OF THE VENTURI THROAT.   THE  WASTEWATER IS COLLECTED IN AIM EQUALl^ATIUN BASIN.  DEPENDING ON




IHt DESIRED  DEGREE OF NEUTRALIZATION, THE  »vASTL«ATtR IS THEN RECYCLED TO THE SLRUBHER OR PUMPED TO




THE rtASTEWATER TREATMENT FACILITY.




    bl-VFRAL  OPERATIONAL  PROBLEMS WERE ENCOONTERED UPuN INITIAL STARTUP.  A SEVERE PLUGGING PROBLEM




.VAS ENCOUNTERED IN SEVtRAL PJMPS DOE To THE  PRtSENCE OF COTTON KIBERS IN THE ftAS TErtA TEit.   4 SCixEtN




rtASKtT  AROUND THE INITIAL SCRUBBER  SYSTFM  INTAKE  PIPE  IN THE DYE COLLECTION  MANHOLE  IS BEImG  USED




11-hPul'AKU.y  UNTIL FURTHER INVESTIGATION IS COMKLE1ED.   SURF ACE-AC TI Vt AGENTS IN THE  DYtl.MG OASTE-




.MAIFRS  VHICH PRODUCE FOAMING IN  THL scRUbHER  PUMP «ERE DETECTED AND  A DEFOAMER ADDITIVE is NOW




INJECTED INTO THE SCRIIBBtR FEED FROM THE DYE  RETENTION BASIN.   FOOLING OF  THE  PH PROSES AND SULFUR

-------
                                                                                     STATUS At, UF 07/30/7H





                                       SECTION   9  (UO.jT It'JUFU)




                          CE  DESCRIPTION FO* UPtRAT lfK»AL  KGu SYSTEMS UN  INOuSTKtAL  dUILtrtS





CANTUN TEXTILES?  CANTdur  GtOriGIA (CONT INilF.i) >






ANU MIST GENERATION  ARE  UTHtK KWUHUKM AWtAS THAT  HAVt  HF.tN INVt S T ! G A F EU.









                                          UPEKAI I-NiG HISIOnV




3RD UUAIUER-1977      MO  OPtWAllOiMAL HRUBLEMiJ  WtKt iVFKUkltO DURING THIS  SukvFY PEHIUD.   THF. PLAiMT




KEHORTS  THE  SYSTEM IS rtOKKINii bA TI bFAC I OK H Y .   ThF. PuANT HAS HtEiM dllKNlNG iMAfll^Ai. GAS bUT  EXPtCTS




TO RETURN  TO COAL DUKTwG THE HEA1ING  StAbON (OtCtMBEH-ilA 1) .






4TH UlJARIEH-1977      I>(E PLANT STAKltO  HURnlMG CuAu AMU OPERATING SCHUiiHER 100 PtRCEmT  OP  (HE  TIME




IN MID-OCTOBEK.   NO  OPtMA T iU.MAL PRUHLEMS HAVt  BEEN £M JIJ.U EKEO DuBI'MU  IHIS PEhlOO.







1ST QDARTEH-1978     THE  SCWllbBtR OEMONSTRATEO  AN OPfKABlLlTY OF  100X.






£NQ QUARTEK-1978     THE  SCKIJttBtR WAS  SHlJTDOrt.M IN MID-MAY WHEN  GAS FINING HESUHEO FW SUMMEH.   COAL-




FIRING WILL  RESUME IN MID-OCI.  OUHTNG  CUAL-HKED OPERATIONS IN  1977  AND 1470, THE SCNUBHE*  WAN  AT  A





100X  IJPEKABILIIY.

-------
                                                                                      STATUS AS OF 07/.30/7B
                                         StLTKliv   9 (CONTIMJFLJ)
                  P£RFU«i,AMCt DESCRIPTION  FOK  OPERATIONAL FRu SYSTEMS UN  INDUSTRIAL  BUILERS
   INSTALLATION  NAME
   INSTALLATION  LUCAT10I-:
   SliuRLfc  CHARACTERISTICS
   SOuKCE  HATING
          OF SEPARATE  Fi,D UMTS
          CAPACITY
         L SYSTEM VENDOR
           PROCESS
   i»E« / RETROFIT
   START-UP DATE
   CONTROL SYSTEM STATUS
   SOd EFFICIENCY
   SLUDGE OR BY-PRODUCT DISPOSAL
          AK TRACIOK  c:o.
 cAST PEOKIA, ILLINOIS
 COAL (i.d% SULFUK)
 e!lO,OOu-3CFM (IOIAL  - 4  BOILERS)
 aO,OOfl ACFM ol i5o F, FUH  EACH  OF  «  FSD SYSTEMS
  u
 100 MW (EQUIVALENT); TOTAL  - 4  ROILEKS
 FHL ENVlKOiv^tNTAL EUUIPMENT
 DOUBLE ALKALI  CCONCEINTKATEU)
 £  NEft,a KEIRUFIT
 APi
-------
                                                                                   STATUS AS OF  07/30/7B





                                      SECTION  9 (CONTINUED)




                PERFORMANCE  DESCRIPTION FOR uPLk A I 10<\ AL FGu SYSltM&  UM  INDUSTRIAL  HOil-tRS
  INSTALLATION  NAME




  INSTALLATION  LOCATION




  SOURCE  CHARACTtRlSTICS




  SOuP-CE  RATING




  f«Oi«.htK  Oh  SEPARATE FGO ONUS




  snuPLE  CAPACITY




  CONTROL SYSTEM VENDOR




  CONTROL PROCESS




  i-iEft /  RETROFIT




  STAPt-oP OATt




  CO.JTKOL SYSTEM STATUS




  S0
-------
                                                                                    STATUS AS (IF 07/40/78
                                       SECTION  9 (CONTINUEU)

                 PERFORMANCE  DESCRIPTION FOR OPERATIONAL. FGD SYSTEMS UN  INDUSTRIAL  BOILERS

CATERPILLAR  TRACTOR  CO.;  JULIET,  ILLINOIS (CCiNI INUED)


THE UNITS  WERE  ULTRASONICALLY  1ESTEU Awn RESULTS ShOrt 1HAT THE SYSTEMS  AWE UN  IHt  HIGH

SIDE OF  IOLERANCE  LEVELS.  A  M1NUR  LEAK WAS DElECltO AS A RESULI OF A FAULTY fttLu.


tTM UUAR1ER-1977      F&D  SYSTEM  RESTART UCCUKREO AT THt BEGINNING UF THE HtATTiMb SEASON.

PLANT HAO  INITIATED  A  PROCESS  OF  DETAILEu (JECUKO KEEPING  HuT ftftS ST TLL  *UKK 1 Nr,

ON THE INTERNAL  INFORMATION  TRANSFER PROCESS.   PLANT HAS  IwRI.CATfcO THAI A SUMMARY  OF  THESE

RECORDS WILL BE  AVAILAbLE  TO  THIS REPORT IN IHt NF.AH FUTURE.


1SI UUARTER-1978   FILTER  CLOTH  PRUBLEMS CUNTlNUED  WITH KEPLACtMtNT BEING KEUl'lRtO EVERY  8-.1  hEEKS.

THE SYSTEMS WERE OOrtN  IN  MARCH BECAUSE  OF HLUGtEu
2ND LHIARTER-1978   UNRELIAbLt  SOi  MQNIIORS  WtRt  A KRuBLEM DURING THIS PERIOD.  Ht.AV Y ' ATTKI F ION  OF
FILTER CLOTHS CONTINUED.

-------
                                                                                   STATUS Ah OF





                                      SELIUiN  1  (LONTINiUFIj)




                PERFORMANCE DESCRIPTION M)« UPtKATIONAL  FGU  SYSTEMS  UK  INDUSTRIAL oOJLEKS
  INSTALLATION NAME



  INSTALLATION LOCATION




  SOURCE CHARACTERISTICS



  SOURCE RATING



  NUMrtER 01- SEPARATE FGO UNITS



  SOORCE CAPACITY



  CONTROL SYSTEM VENDOR




  CONTROL PROCESS



  NEW / RETROFIT



  START-UP DATE



  CONTROL SYSTEM STATUS



  SOd EFFICIENCY



  SLUDGE OR BY-PRODUCT DISPOSAL
CATESP1LLAK IRACfOK CO.




MORTON, ILLINOIS




COAL li.i* SULFUR)




40,000 t>UFI»i ITUT«L ~d ttOlLERS)




 S




20 Mn  Ifijll IVALtNU ; TOtAL  -   TECHNOLOGY.   THE  TrtO  BulLERS  AND THE TrtO SCRUBBING TRAINS AND t»OST  ANCILLARY




EQUIPMEM ARE WITHIN TnE BOILER rtOUSE.




   THE SYSTEM AT MORTON IS VERY SIMILAR TO  THAI  AT  THE CATERPILLAR JOLIET PLAf T, WHICH HAS  BtEN




OPERATING EACH HEATING SEASON SINCE  OCIOBER  1971.   WHENEVER POSSIBLE, PROBLEM AREAS  AND




SOLUTIONS IDENTIFIED IN JOLIET OPERA] IONS  HAVE  BtEN IMf-LtMENTEli TO IMPROVE THE  SYSTEM DESIGM




AT MORTON.  SPECIFIC AREAS IN WHICH  MOUIF 1C AT IUNS  TO  DESIGN HAVE BtEN MAUE ARE  WATER BALANCE,




HUMPS, PH MONITORING, PIPING, LIME  S10RAGF:,  AND COLD  AtATHtR PROTECTION.
                                          OPERATING HISTORY




1ST UUARTER-1978     SYSTEM  START-UP  OCCURRED AT  THE BEGINNING UF JANUARY.   INITIAL  OPERATIONS WERE




PROBLEM-FREE.  THROUGH  JANUARY  AND  PART  OF FEBRUARY, ZURin PERSONNEL WERE TKAIMNG  THt  bOlLER PLANT




PERSONNEL  IN THE OPERATION  OF  THE  FGi) SYSTEM.  OPERA I TufMAl EXPERIENCES  A1  jOLItT  AND MOSSVILLE HAVE




SHOWN  IHAT THE BOILER OPERATORS CAM  BE EFFECTIVELY TRAINED Tu uPtRATE AND  MAIMAIN  THE Fbl) SYSTEMS.




CURRENT PLANS CALLED FOR  ACCEPTANCE  TESTlNb IN THE SPKINo, BuT  TnE CUAL SITUATION  MAY  UELAY THE IFST




PER1UO.






rf
-------
                                                                                      STATUS AS OF 07/30/78
                                        SECT 10.,   9  (CONTINUED)
                              OESCrflPTiOr. Kit. OPERATIONAL  hGu  SYSTEMS UN IM>USIMAL  BOILERS
   INSTALLATION NAME
   INSTALLATION LOCATION
   Si'URCE CHARACTtRlSUCS
   SOURCE RATING
   MIi-irtcR Oh SEPARATE Flil)  UNITS
   SOURCE CAPACITY
   LOi.TROL SYSTEM VENDOR
   LOiVTHOL PROCESS
   
-------
                                                                                   STATUS AS OF 07/iO/7t>





                                      SECTION   9  (CONT INUED)





                PERFORMANCE DESCRIPTION (-OR  OPERATIONAL  FGl)  SYSTEMS ON TNDUSTKIAL BOILERS





CAIFitPlLLAK IRACTOK CO.; MOSSVILLE,  ILLINOIS ICONTINuEO)
AriuVt PrfuCtSS LIQUID



     SL'Jufit HANDLING - SLOdGt  IS  TRANSPORTED  FKOM THt  VACUUM FILTERS TU THE LOADING AREA ON A BELT




CCihVtYuR.  SEVERAL STRATEGIES,  ALL  IfcVOIvIiMG  SCRAPING  OR PLUrtliMG THE DEAATERtD SLUDGE UFF  I Ht BFLT,




KfcSllLTtO IN tXCESSIVE rtEAR Oh  EITHER  THE  BtLTS  OK I Ht  HLUWS.  THE PRESENT APPROACH SIMPLY  OUNiPS




IHt HAItxIAL OFF  THE f-NO OF  1HE  HEU  INTO UINS.   THE PUS1T10IM UF THt BELT' IS CHANGEABLE SO ThAF




ElbHI -41NS CAN BE FILLtO BEFORE  THEY  MUSI  BE  EMPTIED.  A FUkThiEK MODIFICATION HAS A DUAL POSITION




CHuTt uNOEK EACH  HtLT tMO POSITION,  SO  THAT  A lOTAi.  OF 16 blfcS CAN BE PLACED ON IT AT A IIME.




SLUICE BINS ARE THEN LOADEO  HYIJRAULICALLY INTO  TRUCKS  AND nAuLEO TO THE SANITANT LANDFILL  AREA.




ANuTrtEK HR08LEM,  COLD AEATHEM  ICING  ON  THE SLUUGE LOADING AREA, rtAS SOLVED BY ENCLOSING THE AREA.




     INSTRUMENTATION - Ohi^tMAL  DESIGN  PLANS  CALLED  FOK GONTKOL BY THE MONITORING OF  THE so3/sot




KAflO AND SODIUM  ION CONCElMTKATION.   THE  CONTROL RANGE WAS FOUND TO BE TOO SMALL AND  THE PRESENT




APPROACH IS PH CONTROL (6.5)  AND  CLEANING UF  ThE PROBES EVERY OTHER DAY.




     ORIGINAL DESIGN DID NuT MONITOR  S02  CONCENTRATION BUT A COMPLETE MONITOR SYSTEM  WAS INSTALLED




PRIDK 10 THE 1977-78 SEASON.



     PIPING - MODIFICATIONS  HAVE  BEEN MADE WHICH FACILITATE CLEANING OK SCHEDULED REPLACEMENT.








                                          OPERATING HISTORY




<4TH UOARTEW-1977    CATERPILLAR BEGAN A PROCtOUHt OF DETAILED RECORD KEEPING, BUT THE FLOW OF




INMIKMATION rtAS NOT YET  SULH THAT IT  WAS  AVAILABLE TO THIS REPORT.






dfJO UMARTER-l<'7ft   NUMEROUS  BOILER-RELATED PROBLEMS HAVE COMPOUNDED FGD SYSTEM PROBLEMS.   MAJOR




KGii PKGBLEM AREAS WERE AS FOLLOWS!




    tWuSlON OF SCRUBBED  LINER  MATERIAL.




    EXCESSIVE «EAR OF PIHING,  PUMPS,  AND  CONTROL VALVES.




    SLUOGE FKEEZE-UP ON  IHE  CONVEYOR BELT PLUGGED SLUOGE CHUTES.

-------
                                                                                     STATbS  AS  UF  l)7/30/7b
                                        SECTION  9 (CONTINUED)
                  PERFORMANCE  DESCRIPTION FOK OPERATIONAL FGD SVSTtMS ON INDUSTRIAL  BOILERS
   INSTALLATION  NAMt
   INSTALLATION  LOCATION
   SOURCE CHARACTERISTICS
   SOURCE RATING


   NUMBER OF SEPARATE FGO UNITS
   SOURCE CAPACITY
   CONTROL SYSTEM VENDOR
   CONTROL PROCESS
   NEW / RETROFIT
   START-OP DATE
   CONTROL SYSTEM STATUS
   S02 EFFICIENCY
   SLUDGE  OR BY-PRODUCT DISPOSAL
   CONTROL SYSTEM CuSI
 CHtVRON  U.S.A.  INC.
 BAKEkSFIELU,  CALIFORNIA
 UIL  11.1%  SULFUR)
 c>Ub,OOo  SCFM  (TOTAL  -  1* BUILERS)
 150,1/00  ACFM  ;i  500F, FOR EACH UF 5 FGD SYSTEMS.
  3
 90U  MM HTU/HK  (TUTAL -  18 BOILERS; fc BUILEkS/ FGD SY.STtMj .
 85 M«  (EQUIVALENT);  VOo MM B1U/Hh: luTAL - le flOILERS
 l?i>  hW  (EQUIVALENT), TuTAL - 1 tt BOILERS
 KOCH ENGINEERING
 SODIUM CARBONATE scRuRtsiNG
 RETROFIT
 JULY, 1978
OPERATIONAL
90*  (7U PP^: at OUTLET)
HASTEWATER TREATMENT AND  DISCHARGE  TO  TAILINGS POND
CAPITAL:^,BOO,ooo (1979).   THIS is  TOTAL  INSTALLEU  COST
OF THE FGD SYSTEM, INCLUDING  SITE  PKEPATION.
                                           OPERATING: APPROXIMATELY  $90o/oAY  PER  SCRUBBER ti97b) .
                                           THIS CORRESPONDS TO A  TOTAL  OF  *  9dO,OuO/YR K'R  ALL -THE
                                           SYSTEMS a/ i«0 UAYS/Yk.  THE  COST  INCLUDES  ELECIRICITY,  SUOA
                                           ASh, AND MAINTENANCE  (LABOR  AND MATERIALS  ).
                                        BACKGROUND INFORMATION


     CHEVERON  U.S.A.  HAS  AN  UIL  SITF  AT b AK EkSF I ELU , C AL 1 1- ORN I A . THERE ARE ABOUT  bl)  STEAM  GENERATORS
      6URN  l.U  SULFUR  CRUDE  OIL.  EACH  GENERATOR IS RATED AT 50 MM BTU/HK. THE STEAM  Is USE!'  1 u  HEAT
OIL ANu hACILITATE  ITS  FLOn  UPWARDS  ^UM THE  OIL WELLS.
     KuCH ENGINEERING HAS  COMMISSIONED  THREE  FGO SYSTEMS IN JUNE/JULY 19/8.  THE  SODIUM CARuONATE
SCRUhMNG PROCESS IS  USED, WITH  EACH  SCWUHBFk TREATING FLUE GASES FRON b GENEf-'AlURS WITH  A  TuTAL
FLOW RATE OF 150,000  ACFM  AT  5uO F.  THERE ARt 3  MICH  FLEX I fk AYS AND A KOCH FLEXlMESH  DfcMlSIER  IN
tALh SCRUBBER. THE  SPENT LKJUOk  IS MIXED !«' 1 1 H f-RESn SOuIUM  CARBONATE IN THE uOITOM  OF  THE SCRUBBER.
A CONTiNuOOS BLEED  OFF  STREAh,  IS TAKEN  Tu D I SPOS AL POND ,  .'.HLREAS KEST OF i Ht LTuUuW  IS KE C IkCUL A TtO .
A PH OF  b-b.5  IS MAINTAINED AT THE TUP  T * A Y AND  A  L/li RATIO UF  S GALLON'S/ 1 000 ACF IS  USEcJ.  THERF Is
iMO REHtA)  FACILITY  BUT  THE SCROBuFR LAN  bE BYPASSED.  TnE  BulLEK l.D. FANS  WILL HE UPGRADED  TO  OFFSeT

-------
                                                                                       bTATUS A6> OF  07/jtl/?U
                 PERFORMANCE UF.SCKIP1 lOiv F- ON uPfc R A T i flNAL F-Gu SYb'tMb  UK I iMPuS I l> 1 AL  BDllekM




CHEVRON U.S.A.  liMC.; rtAKLRSF ItLO,  CALlhtlKfjIA  (CUM iNotn)






THt HHESbUKE  DKOP UF 1 IN. ftU.  TuE hLKUBHEKh  AKE  PtSlGnF.-  10  Rf-uVt  >*IU UF  SUH  Auli MAINTAIN  t. X i 1  Su2




COivCENTRATlbN BELOW 7U PPM. tACH SCKUBtsEH  IS  1 h . •s  FT.LT P1A. ANu  ^5 FtM HIGH.  I Ht  HflKuT  INCLUDES




IHAT OF A  STUB  STACK SITjATEi)  UM TOP Oh tALK  SCRUHSEh.




     THE SCWUBbEKS AM) Tt
-------
                                                                                    STATUS AS OF  07/30/7d
                 PFRFURfcANCE DESCRIPTION H>k  OPERATIONAL
                                                              SYSTEMS UN TNUUSrRIAL UOILERS
   INSTALLATION NAME
   i'MST ALLATION LOCATION
   SOURCE  CHARACTERISTICS
   SOURCE  RATING
   ivUmfitR  OF  SEPARATE FGD UNITS
   SOURCE  CAPACITY
   CONTROL SYSTEM VENDOR
   CO,  300  FJ
 1
i Ml* (EQUIVALENT)
f MC tNVIKOiMMENl AL EQUIPMENT
DOUBLE ALKALI  CCUNCEuTKATED)
RETROFIT
JANUARY, 147b
OPERATIONAL
90.5% CluOO PPM ol INLET)
97.4% CS Lb/MM BIU  S  INLET TO  MECHANICAL COLLECTOR.)
DFnATEWED SLURRY TO LANDFILL
CAPITAL: $163,uoo us7t).  THIS  COST  INCLUDES EQUIPMENT>
ENGlNEERINli, AMD STARTUP.  THE CUSI UOES NOT INCLUDE
LAbOK AND MATERIALS K)H ELECTRICAL  SYSTEM,  PIPING,
OR STRUCTURAL ANU FOUNDATIONS  ERECTION.
                                           OPERATING: sbO,ooo/YR  (1977).   THIS  COST INCLUDES
                                           LABOk, F.LECTRIUI IY, DISPOSAL,  MATERIALS, AND LAB WORK.
                                        BACKGROUND INFORMATION
     THE FIRFSTONt  TIRE  AND  RUBBER CO.  LOCATED IN POTTSHHvN, PENNSYLVANIA  HAS  BEEN OPERATING A FGO
SYSTEM SINCE JANUARY  1975  AS A  DtHUNSTKA11UN-SLALE PLANT, DESIGNED  TO  TEST  THE  FEASIBILITY OF FGO
UN INDUSTRIAL BOILERS.   THE UNIT  is DEMONSTRATING ^o PHRCE.MT Sue REMOVAL  EFFICIENCY  «ITH AN
AVAILABILITY OF  90  PERCENT  AND  A  FLUE  GAS  CAPACITY Oh 12!,000 ACFM OR EQUIVALENT  OF  3.0  Mw.  THIS
FLO« REPRESENTS  APPROXIMATELY  1 /.4 THE  TOTAL OUTPUT OK UNE 120,000 LB/HR STEAM BOILER.   THE SULFUR
uluxii.t EMISSIuM REGULaTHJN FOR  THE KLANT  IS O.«b Lhb /"I I LI. I UN ulu OF HtAI OUTPUT.
    THt PLANT IS USING  THE  CONCENTKATEu OOOHLE ALKALI PROCESS PATENTED BY FMC CORPORATION.  THE LOAD
CAPACITY f)F THE  bOILER  Oi\,  fiUlCti  THE SCKUdfltK IS jPERATINb IS APPROXIMATELY  ID rtW.  IN UCIObER 1976,
int. oUiLtR WAS CONVERTED FROM BURNING  KEStOUAL FuEL ulL 12.354 s) TO COAL  (<».S-i.OX  S) .
    IKE vENTURl  SCRUHBER IS SPKAYEO rtllH ALKALINE LIUUUR WHEkE THK FLUE GAS ENTERS.   THE FAN AND
u*i..PtK UPSTREAM  OF  VtlMHJRI  CONTROL  THE  FLMc bAt> KEtO.  SCRuBblur, LIQUOR hLUWS FROM  THE  VENTURI  TO
THE M'lTTUM OF CYCLONE DEMlbThR  AND  THE'M 1N T (1 THE htC 1RCHL A TI ON TANK.  DROPLETS OF SCRUBBING LIQUOR
A*c ,iPjr» DOT IN  THt CYCLONE AND RON tiACK OOIMM IN i HE RtC I RCUu A TI UN, TANK.  THE SCRUBBING  LlJUOR  IS
PAf,TLY RECIRCULATEO TO  THE  VEiMUIKl  THUS LUhPLETlNU THE SCRuHoIuG CYCLE.   ACCUMULATION OF SULU3LE

-------
                                                                                   STATUS AS OF U7/30/7B





                                      SECTION   •»  (CONTINUED)




                PERFORMANCE DESCRIPTION  K)K  OPERATIONAL  FGU SYiTEMS ON IiMHUSTWIAL BOILERS





FI-*.




 4TM JHAHTEH-J976     IN OCTOBER.  THE  SYSTEM UPEKAfED AT A RELIABILITY  INDEX OF  IOOX,  UNTIL THE UNIT




 *AS CONVtMTEu TO  COAL  FIRING  U.5  -  i.0% SULFUR).   THF SYSTEM OPERATED FOR AN ADDITIONAL  511  HOURS,




 OF  THE  «6 H£UUIkEO, OEMUNSTRATHMG A RELIABILITY IiMDtX VALUE OF 97.2X.   IN NOVEMBER  AND DECEMBER,




 IHE SYSTEM OPERATED  F0n  1172  HOURS AGAINST THF. REQUtrtEMEiMT OF  1211 HOURS.  THEREFORE, THE AVERAGE




 RELIABILITY  INllEX  FOR  IHE TrtO MONTHS WAS 9b.7%.




 1SI uiUAKlEK-1977     SYSTEM OPERATED 1193 HuUkS, flAS kEUUIREO  Tu UPERATE  FOR  14b9 HOURS, YIELDING A




 Ktl. IAH1L1TY  1NUEX  VALUE  OF  81. CX.   SYSTEM WAS DEalbNtO FOR A  MUCH  LOWER  PARTICULAR LOADING THAN
                                                   til

-------
                                                                                   STATUS  AS  OF  07/30/78
                                       SECTION  9 (CONTINUED)
                 PERFORMANCE DESCRIPTION FUR OPERATIONAL fSO SYSTEMS UN INDUSTRIAL BOILERS
 FIRESTONE  TIRE AND Ru«bER CO.  ;  POTTSTUWN,  PENNSYLVANIA CCuNTiNUtO)

 THAT  ACTUALLY  ENCOUNTERED ON CUAL FTKING.   THE HIGH GRAIN LOADING CAUSED ABNORMAL «EAR AND DOWNTIME
 UF  THE  F.D.  FAN.

 dNO u.UARTER-1977     SYSTEM OPERATED  139fl  HOURS,  WAS RETIRED Tu OPERATE 1690 HOURS,  YIELDING A
 RELIABILITY  INDEX  VALUE  OF 8
-------
                                                                                     STATUS  AS Ul- 07/30/7B
                                       SECT 10 IV  •?• tClli.T IMOKO)




                PERFORMANCE OFSCRT('T I»IM I- Ol< Ol't R A F I fi .. « L  K(i,j  SY.iTcMb J.v I '< I AU
  INSTALLATION NAME




  INSTALLATION LOCATION




  SOURCE  CHARACTERISTICS




  SOURCE  RATING




  NUnRER  OF SEPARATE FbO  UNITS




  SOURCE.  CAPACITY




  CONTROL SYSTEM VENDUK




  LllNTHOL. PROCESS




  ME in / RETROFIT




  START-UP DATE




  CONTKOt SYSTtM S'lAHJS




  SOI EFFICIENCY




  PARTICULATE EFFICIENCY




  WATER MAKE-UP




  SLUDGE OR BY-PRODUCT  DISPOSAL
  CONTROL SYSTEM  COST
(•ML l5t(l)A ASH  HI. AND




l,KEFIM n'lvtKt 'AYUMlNG




LllAL (I'/- Slll.nJ'O




'»ae,uoo SCFM  (loiAL  - d
c>.S(j Mw  ItUUltf AUh'iJTJ :  TOTAL - c1 1-UJlLfcRS




FML ENVlKUlMMtNT AL  EMUlPMtNf




S'lOIUM  CAKnOmATF  SCRUHtflM5




Nfcrt




MAr ,  I47h




UPtHATlOMAL




9S* IBOO PHH  AT  INLET)




REMUVEIJ bY  PRFCF.UING FSP  (49. 5«)




OPEN  LUDP*  L/6 -  lb-c!0 GAL/1000  ACF




HOL01NG POND  FOR  EVAPORATTUN




fMAriSOJ/Soa  L1HJOK DISPOSED TO  COLLECriUN PONU - MO PKIU*




AEKAIIUiM.   LANDFILL IN ThF. FOToRL




CAPITAL COST  INCLUDES tSP
                                        BACKGROUND  1NFOKMATION




    FMC CHEMICAL  CORP.  HAS A SODA ASH PLAN1  IN  GKELM RIVtR, nYOMIiMli.   THE  PLANT HAS TWU COAL-FIRtD




POWER BOILERS WHICH  BURN 1.1 PERCENT SULFUR  COAL.   THE FLUE GAS HRUM  EACH  BOILER (330,000  ACKM  AT




320 F) IS TREATED 8Y  A  HUTSIDE FSP WITH 2flh  r-'LATCS Ai\D A PARTICULAR  HEMutfAl. cKFICIEiMCY uF  99.5  %.




    THE FLUE GASES ARE  SCRUBBED BY THE PLANT ENO-LIOuOR IN TWO SCRUBBERS,  EACH WITH THKEt  PAIRS  OF




DISC-AND-OONUT  THAYS.   THE SCRUBBERS AND  1 HE DISCS A«E LINED WITH CEILCOfE Io3 rtHEnEAS  THE  DONUT




PAKTS OF  THE TRATS ARE  MADt FRUM  IMCUNEL  8cb.   THE StKUfibtrt LIuUoH  IS MAINTAINED Al A PH OF  6.3  ANu




IS RECIRCULATED AT A  RATt OF 10 - IS GALLONS/1 oOl)  ACF OF FUJt bAS.   A PAKT OK  FHt REcIRCULAT ING




LIQUOR IS CONTINUOUSLY  PURGED 10  REMOVE SULFITES AND SuLHAItS FUrtMEll  BY  IHt rttACTIUN OF oOa  .HFH




SODA  ASH.   THE  RECIRCOLATING PUMPS AND THE RELATED PIPING  IS RUHBER  LIiMFU.  A  HESH  TYPE uEMlsTfc'R 15




USED  IN EACH SCRUBBER.   THE bASES ARE REHEATED  BY  OTRELT FlRi,Mb OF  NATURAL GAS Al  IHc EXIT  UF  IHE




SCRUBBERS.  THE REHEATED FLUE GAS IS MIXED 'U1H HYPAoStt) GAS BcFjRt  bUliMG  TO THE STACK  AT  ArtulIT




180 F .




    AUTOMATIC  CONTROLS  MAINTAIN SOLUTION  LEVEL  If-  IHt bCRUBHER BASIN.  THE HRIrtAWY  SOURCE  OF




MAKE-UP IS  PROCESS WASTEwAlFn nHICn  iS CHANNELED Tu  A MAKt'-up  IA,gK.   I(-  MilKF f'AKt-oP  IS REuilI




WIVER WATER IS  TAPPED.   IHE SCKUI3&EK BLEED STREAM  IS PIScHAKliEli  in  A  WASIF PUM)  »T  IHH  SITt.




DAMPERS «ITH REMOTE CONTROLS REGULATE  IHE (-LOW  OF  OFF tiAS  fHKOUGH  AND AhuUnD 1 HE SCRUHBEnS.




APPROXIMATELY  5>OI OF loTAL  FLUE GAS  IS ROM THKlUbH  TnF  SCRofluFKS.

-------
                                                                                     STATUS AS UF  07/30/7a
                                        SF.CMOu  f ICIIivT llMUf L>)

                 PERFURNANCt UFbr^THUdN  Ff,K ,.Pt R A . I Hiv AL h Gl, SY^TtMb  UN  I,,DUSl«tAL BUILEHS
     (SUI.» ASH PLAN!); (,H|tF.N Klvt(v,  ,,Yl-)Mm, (u
                                           UPFnA, Fur; HIS I DRY
 JRD  uUAR.ER-1,77     M,»E PROBLEMS HAVE OCCuKKED  «I,H TnF SuRUflBKK LINING  AS  A  RESULT OF FAULTY
 INFLATION.   THE POSSIalLl.Y OF RHNNIN,  ,HE  SYSTtM W1TM Nf, RtH£AT  IS RtlN6  !.VESTIGATEO.

 ,TH  HUA,IE«-1977     THt SCKUB8ERS HA«E CoK'ROUEU  AS A RtSULT UF FAULTY INSTALLATION OF  THE LINING.
 IHt  IMPURITIES  IN  THE  SCRUBBING LIUUUR CAUSE FOAMING AND SEDIMENTATION ON THE  TRAYS.

 IS,  UUARIE«.,,78     PIPELINE FREE7UPS. AND LEAKS  FROM I HE VANE HAMPERS WERE  THE  MAIN PROBLEM AREAS.

«*u  UUARIEft-197e     IHt DEMISTER ,AS PLUGGED,  ANU  , HE  RFCIRCULAUON PUMP WAS DOWN  FOR  SOME PERIOD.
PH CUMKUL  IS N01  VERY  EFFEC.IVE,  CAUSING PH ExCtRSION,  ,0 A.OuT  ,.».  THIS HAS  CAUSED  SCALING IN
 InE PIPELtNES AND  IN THE  TO.VER.  F,C TESIS HAVE MEASURED S02 REMOVAL EFFICIF.Cr  IN  IHE  RANGE OF  87%.
^1%,  flEPtNuING ON  L/b  AND  PH.

-------
                                                                                            AS uF
                                       sf uT ION  <>  (LONT
                PERFORMANCE INSCRIPTION FOR UPt R A T 1 ON A I  FGu bYbTtMb UN  I IMllUS f WI Al. BOlLtRS
 1'iSIAI.LATlON  NAME
           IUN  LOCATION
         CHAKACURIS1 U.S
         RA11NO,
 INIMHEP  OF  SEPAkATE FbD  UMIIS
 aiii)Wi.E  CAPACITY
bEiMEkAL HOIHRS  CORHOHA riurj

DAYTON, OHIO
CUAL10.7*  -  cJ.uX SULHIRJ
ih,l)00 SCFM  UOTAL - .TrN bYPASS THE  GASES TO IHE ATMOSPHFi-E  IN CASE OF A  SCRUBBER
MALFUNCTION;  OR IT CAN MIX AMBIENT AIR MIH  IHE FLUE  PASES IN CASE OF  LO« LOAD IN OROER  10 MAINTAIN
CO,\SFAi\iT  AIR  FLO»* 10  TnE  SCKUbbER  FAN.
     THt  hCKUHBER CONSISTS OF  THE  F.NTULETEW  "VA^E-CAGb"   (b Fl. I) IA. X  <, FT. HIGH) rtHlCH IS HOUSED IN

-------
                                                                                     STATUS AS UK
                                         SECTION   g  (CONTINUED)
                  PERFORMANCE DESCRtPTIO, FOR  OPERATIONAL  FGO  SYSTEMS UN INDUS, RIAL BOILERS
  GENERAL MOTORS CORPORATION; DAYTON, UHIO  (CONTINUED)

  A CONICAL BOTTOM SEC.ION (» FT. DIA. X 5 FT. H1&H), AN TNTERMEDIATE 8ECT,ON  („ FT. DIA. X
  5 FT. H,6H)f AND A DISENGAGEMENT ZONE  do FT. UTA. X  1,  FT. MlliHJ.   THE  FLUt  (,AS (i4,0u0 ACFM
  - 50UFJ  ENTF.RS THE BOTTOM SECTION TANGENT I ALLY .  RtCIRCULATIuG LIQUOR  IS  SPRA,tU FROM THE rOP OF
  !HE  VANE CAGE SECTXON,  WHICH CAN BE MOVED  VERTICALLY  TO  VARY THE PKFSSORE  URuP ACRUSS THE ttc»U88tH
  A PRIMAL  UEMISTER IS LOCMED ABOVE ,Ht PREVIOUSLY MENTIONED I.TERMEUUTE  SECTION ANO A SECO^OARV
  UE.ISTER IS  LOCATED ATOP THE OI8£N«BtMEMT ZUNt.    IHE  G4b , HtN PASStS  .HKOJGH  A ,TuH  STACK  Tu THt
  AT.nSPHFRE.   SCRUBBING  LIOUOR IMH,NRtS ON  , Ht b01TOM OF  THt VA,,£ CAGt  ANU  A SPKAr CHAMbE, tFFFCT
  H«UV1,,£S THE S02  REMOVAL.   SCRUBS UNUFKFLO-,  CONTAINING PARTICULAR  ANO  A ,^SoVSu<  SOLUTION IS
  SENT  TO  ,HE  RECYCLE TANK,  HHtRE HAKEOP ,ATt, AT A   RATE OF ,0 GPM IS ADOC,,.  RECYCLE  PUMPS  TAKE
  LIUHOR FROM  THE  IOP OF  THE  RECYCLE  TANK, ALONG  WiTH ,HE CAUS.Ic STREAM A.OLD Tu  TH, FEED  LINE,  ANO
  KEdKCOLATE  IT TU  ,HE TOP  OF  THE  VANE  CAGE  AT A  RATE  OF  ,00 BPM.   THE L/G ,75     THt  DAMPERS ANO OAN.PER  CONTROL  SYSTEMS WERE MAJOR PROBLEMS.   THREE SETS  OF
 EXPANSION JOINTS  HAD Tu  BE  INSTALLED BEFORE ACHIEVING PROPER FL0« CONTROL.
 MU yUARTEK-i47i     A  FAN BEARING  HAD  .0 BE  kEPLACEO THRtE TIMES.
 iRD ^OARTEK-1975     INSTRUMENTATION AND  CONTHOL  PROBLEMS PkOHPTEo  WIRING REVISIONS.
 «TH UUARTER-1976     T HE  FGD  SYSTEM  DEMONSTRATED  AN  AVAILABILITY OF 93 PERCENT.
 IS, UUARTER-1977     MECHANICAL  PROBLEMS  WITH  THE  VANE  CAGE DRIVE.   THE ACCESS OOOR  DEVELOPED LEAKS
 AND .HE LIQUOR CORRODED  THE  OUTER  SURFACE OF  THE  INLET  ,,UC ,  AROUuD THE ACCES, DOOR.
4TH UIIARTER-14J7     COKROSION  AND PLUGGING  PnObLEMS  CONTINUED  10 HAMPEK SCKUUHtH  OPERATIONS.
HO.FVER,  USUALLY WHEN A  SCRUBBER IS  UO»N, THE  uTHEK  .OILER IS  FIHEu  OP «H,LE ..PAIRS AKt: MADE  TO  THF.
UtJrtNtl) UNIT.
isi
                    THE PRIMARY UEMTSTER WAS SEVERELY  CORRODED  OOF  TO  ACID DROPPING UU*N ONTO IT

-------
                                                                                  STATUS AS OF 07/30/78
                                      SECTION  9 (CONTINUED)
                PERFORMANCE DESCRIPTION FOK OPERATIONAL FGO SYSTEMS ON INDUSTRIAL BOILERS
GENERAL MOTORS CORPORATION; DAYTON, OHIO (CONTINUED)

FROM THE UPPER DEMISTER.
2ND QUARTER-1978    THt FOLLOWING SYSTEM MODIFICATIONS WERE BEING PLANNED: THE  IIMTERMEOIATE SECTION
WILL BE REMOVED, THE PRIMARY DEM1STER WILL Bt REPLACED BY A SIMILAR VANE-TYPE HASTELLOY-G  DEMISTER,
THE SECONDARY DEMISTER WILL BE REPLACED ttY A RADIAL VANE HASTELLUY-G DEMISTEH,  AND  A CONVEX
IMPINGEMENT BAFFLE PLATE OF HASTELLUY-G rtILL BE INSTALLED ABOVE  IHb PRIMARY  DEHISTER TO  ASSIST  IN
RAPID DRAINAGE OF THE ACID DROPLETS.

-------
                                                                                  STATUS AS OF 07/30/7a
                                      SECTION  9  (CONTINUED)
                PERFORMANCE DESCRIPTION FOR OPERATIONAL FGO SYSTEMS ON  INDUSTRIAL BOILERS
  INSTALLATION NAME
  INSTALLATION LOCATION
  SOURCE CHARACTERISTICS
  SOURCE RATING


  NUMBER OF SEPARATE FGO UNITS
  SOURCE CAPACITY
  CONTROL SYSTEM VENDOR
  CONTROL PROCESS
  NEW / RETROFIT
  START-UP DATE
  CONTROL SYSTEM STATUS
  SOd EFFICIENCY
  PARTICULATE EFFICIENCY


  WATER MAKE-UP
  SLUDSE OR BY-PRODUCT DISPOSAL


  CONTROL SYSTEM COST
GENERAL MOTORS CORPORATION
HAKMA, OhIU

COAL  C2.bX SULFUR* 7.1% ASH* 13,350 8TU/L8)

128,400 SCFM 51 7U F ITuTAL - 4 HOILEKS)
320,000 LBVHR STtAM (TUTAL)
 1

32 Mi*. (EQUIVALENT); TOTAL - 4 bOILERS

GM ENVIRONMENTAL
DOUBLE ALKALI (DILUTE)
RE1ROFJT
MARCH, 1974

OPERATIONAL
90% 1800-1300 PPM a INLET)

63X (AT INLET: UNITS 1&2 - 1.75 LB/MIN* UNITS 3&4 - 1.32
LB/MIN)

CLOSED LOOP

DEWA1EREU SLURRY TO LANDFILL

50 + X SOLIDS (CASU3/SU4) SLUDGE TO DRYING POND AND LANDFILL
OPERATING COSTS ARE $643,500/Y« ol 55,000 TPY OF COAL
                                       BACKGROUND INFORMATION
   THE CHEVROLET PARMA PLANT OF GENERAL MOTORS IS LOCATEU NEAR CLEVELAND, OHIO.  THE PLANT HAS FOUR
SPREADER-STOKER BOILERS FIRED BY TRAVELING GRATES, CAPABLE OF PRODUCING A TOTAL OF 320,000 L8/HR OF
STEAM OR APPROXIMATELY 32 MW OF EQUIVALENT ELECTRICAL CAPACITY.  THE COAL FIRED IN THESE UNITS
ORIGINATES PRIMARILY FROM THE SOUTHEASIERN PORTION OF OHIO AND HAS THE FOLLOWING AVERAGE
CHARACTERISTICS: HEAT CONTENT OF 11,300 BTU/LB, SULFUR CUNTENT OF 1.7 TO 2.7 PERCENT, ASH CONTENT
OF 6.8 TO 14.8 PERCENT, AND A TOTAL MOISTURE CUNTENT OF 0.9 TO 7.8 PERCENT.
    THE POWER BOILERS HAVE BEEN FITTED WITH AN EMISSION CONTROL SYSTEM CONSISTING OF MECHANICAL
COLLECTORS UPSTREAM OF A DILUU DOUBLE ALKALI SCRUBBING SYSTtM.  THE FGD SYSTEM SCRUBBING MODULES
WERE SUPPLIED BY KOCH ENGINEERING.  INSTALLATION WAS COMPLETED ON FEBRUARY 28, 1974.  THE SYSTEM
CONSISTS OF FOUR SCRUBbERS OPERATING IN PARALLEL.  EACH SCRUBBER CONTAINS THREE BUBBLE-CAP
ABSORPTION TRAYS AND A MESH MIST ELIMINATOR.  THE FLUE GAS RATt IS 61,SOU ACFH AT 393 F FOR EACH OF
THE FIRST TWO SCRUBBERS AND THE OUTLET TEMPERATURE IS 137 F.  THE INLET S02 CONCENTRATION IS 765
PPM.  THE FLUE GAS FLOW RATE IS 58,600 ACFM AT 550 F FOR THE OTHER TrtO SCRUBBERS ANO T'HE OUTLET
TEMPERATURE IS 152 F.  THE INLET S02 CONCENTRATION IS 800-1300  PPM.  OUTLET CONCENTRATION VARIES
FROM 136-220 PPM FOR THE SCRUBBERS.
    THE. SULFUR DIOXIDE CONTAINED IN THE BOILER FLUE GAS IS ABSORBED BY A REGENERATED CAUSTIC
                                                48

-------
                                                                                  STATUS AS OF 07/30/78





                                      SECTION  9 (CONTINUED)




                PERFORMANCE DESCRIPTION FOR OPERATIONAL FGO SYSTEMS UN INDUSTRIAL BOILERS




GENERAL MOTORS CORPORATION; PARMA, OHIO CCONTINUEO)






SOLUTION (0.1 MOLAR NAUH), FORMING A SOLUTION OF SOLUBLE SODIUM SALTS.  THE SPENT CAUSTIC IS THEN




REGENERATED BY REACTING THE SODIUM SALT SOLUTION HlTn.SLAKED LIMt, RESULTING IN THE FORMATION OF




CALCIUM SULFITE/SULFATE SOLIDS, WHICH ARE SEPARATED OUT UF THE SOLUTION.  NEXT, SODA ASH IS




ADDED TO THE SOLUTION IN ORDER TO MAKE UP FOR SODIUM LOSSES AND MINIMIZE THE SCALE POTENTIAL FROM




THE CALCIUM WHICH REMAINS  IN SOLUTION.  THE REGENERATED CAUSTIC FORMED IS THEN RECYCLED BACK TO THE




SCRU6BER FOR ADDITIONAL SULFUR DIOXIDE REMOVAL.  THE CALCIUM SALT  AND FLY ASH SLUDGE WHICH RESULTS




IS DEWATERED AND HAULEU AWAY BY TRUCK TO AN OFF-SITE LANDFILL.






EQUIPMENT SPECIFICATIONS





SCRUBBERS.  EACH OF THE a  SCRUBBERS  IS 10.5 FT  01* X 22.5  FT HIGH  X  11 GAUGE THICK AND  CONTAINS 3




BUBBLE-CAP TRAYS.  ALL THE SCRUBBERS AND TRAYS  ARE MADE OF 316 L  S3.  THE SCRUBBERS HAVE A TURNDOWN




RATIO OF 3 AND ALSO HAVE  A BYPASS DUCT.  THE L/G RATIO HAS A DESIGN  VALUE OF 30  GALLON3/ACF  BUT IT




rtAY BE  VARIED DURING OPERATION.   THE PRESSURE DROP ACROSS  THE SCRUBBER RANGES BETWEEN  8-9  INCHES WG.






DEMISTERS.   ORIGINAL 316  S3 DEMISTERS  WERE  CORRODED  DUE TO CONDENSATION  AND  ARE  REPLACED BY  FLEXI-




MESH  TYPE  POLYPROPYLENE ONES.






RECYCLE TANKS/PUMPS.   ALL THE  4  RECYCLE  TANKS  ARE  MILD  STEEL WITH TAR TYPE  RESIN COATING.   THE  PUMPS




 (TUTAL  6,  £  SPARE)  ARE CENTRIFIGALS  WITH MILD  STEEL  CASING AND  HAVE  RUBBER  LINING.   THE PUMP MOTORS





HAVE  40 H.P.





CHEMICAL MIX TANKS &  AGITATORS.   BOTH  THE  MIX  TANKS  ARE  MILD  STEEL WITH  5000 GALLONS  CAPACITY.   THE




DESIGN RESIDENCE TIME  IS  7 MINUTES.   NEW  AGITATORS ARE  PROPELLER TYPE.   THESE  ARE SPECIALLY  DESIGNED




 TO GIVE HIGHER  FLOW  SATE  THROUGH THE BLADES.  THE  DRIVE RATINGS ARE 5 HP AND 45 RPM.






 CLARIFIERS.   BOTH THE  CLARIFIERS (60 FT  DIA X  14 FT  LIQUID DEPTH) HAVE A CONICAL BOTTOM AND 300,000




 GALLONS CAPACITY.  THE DESIGN RETENTION  LINE IS ABOUT 4 HOURS  AT FLOW RATE OF  1300 GPM.



 VACUUM FILTERS.   BOTH THE VACUUM FILTERS HAVE  500  SO. FT. SURFACE AREA WITH 10 FT DRUM DIAMETER. THE




 URUM DRIVE SPEED IS 0.5 KPM MAXIMUM.






 FILTRATE TANK/PUMPS.  THE TANK (4 FT DIA X 7 FT HIGH) IS MILD STEEL AND HOLDS 660 GALLONS OF




 KILTRATE.   THE PUMPS ARE MILD STEEL, CENTRIFIGAL AND HAVE A CAPACITY OF 300 GPM AT 15  FT. OF HEAD.






 PROBLEMS AND SOLUTIONS



      THE SYSTEM WAS STARTED UP ON FEBRUARY 28, 1974 AND BY APRIL  31, IT HAD OPERATED FOR 264 HOURS.




 THERE  WERE TWO SCHEDULED  SHUTDOWNS DURING THIS PERIOD FOR EQUIPMENT  INSPECTION.  THE SECOND SHUTDOWN




 REVEALED THAT SOLIDS WERE NOT BEING DISCHARGED FROM THE PRIMARY CLARIFIER RAPIDLY ENOUGH.




 AS A RESULT, THE CLARIFIER RAKE JAMMED.  A PIPING CHANGE  WAS MADE TO BLEND  THE CAUSTIC FEED




 IN WITH THE RECYCLE LIdUOR.   THIS HAS IMPROVED PERFORMANCE BUT  NOT  COMPLETELY ELIMINATED

-------
                                                                                    STATUS AS OF 07/30/76
                                        SECTION  9 (CONTINUED)
                  PERFORMANCE DESCRIPTION FOR OPERATIONAL F60 SYSTEMS ON INDUSTRIAL BOILERS
  GENERAL MOTORS CORPORATION; PARMA,  OHIO (CONTINUED)

  THE PROBLEM.   PREMATURE CAKE CRACKJNG IN THE VACUUM FILTERS RETIRED THE PRESENCE OF AN OPERATOR
  DURING  OPERATION.   «.M. ANTICIPATES THAT THE CHANGE TO NrLON FROM POLYPROPYLENE WILL SOLVE THIS
  PROBLEM.   CAKE CASHING  TO  REDUCE  LOSSES WAS NOT  INITIALLY  SUCCESSFUL BECAUSE THE SPRAY WATER
  TENDED  TO  KNOCK  THE CAKE OFF THE  DRUM.   ALTERATIONS IN SPRAY PATTERN AND OTHER MEASURES HAVE
  APPARENTLY  SOLVED  THIS  PROBLEM.   THERE  HAS  BEEN  NO  EVIDENCE OF  CORROSION OR  ABRASION IN ,HE PUMPS
  OR  PIPING.

      THE SYSTEM WAS  SHUT DOWN FROM MAY 1  TO  MAY 26,  ,97,, BECAUSE  OF  UNEXPECTED BUILDUP OF  SOLIDS  IN
  THE  CLARIFIER, WITH  SUBSEQUENT OVERFLOW  INTO  THE SCRUBbER.   THE PROBLEM  WAS  SOLVED  BY  1) USING
  A POLYMERIC FLOCCULATION AGENT TO ATTAIN-BETTER SETTLING AND  2) WITHDRAWING  SLUDGE  FROM THE
  CLARIFIER AT MORE FREOUENT  INTERVALS.   SYSTEM AVAILABILITY  TU THE  BOILER  WAS  87  PERCENT IN  APRIL
  197*,, LESS THAN  10 PERCENT  IN MAY,  AND  100  PERCENT  IN  JUNE,  JULY,  AND AUGUST  AFTER  THE  SYSTEM WAS
  RESTARTED.  PLUGGING BY GYPSUM DEPOSITS  IN  THE OVERFLOW LINE BETWEEN THE  CLARIFIERS  AND IN  THE
  LINE FROM CLARIFIER NO. a TO THE M!X TANKS  WAS CORRECTED BY RELOCATING A  CHEMICAL FEED  LINE AND
 REPLACING SOME PIPING.  THE SYSTEM WAS DOWN THROUGH JULY AND AUG.  1975 FOR REPLACEMENT  OF GRAVITY
 FLOW LINES WITH AN OPEN FLUME THAT CAN BE EASILY  CLEANED.  ADDITIONAL MODIFICATIONS  TO  THE  DESIGN
 AND  OPERATION OF THE F60 SYSTEM HAVE CONTINUED.   THE OPERABILITY !NDEX FOR THE FGD SYSTEM HAS
 INCREASED SIGNIFICANTLY  THROUGHOUT THE COURSE OF  1976.  THE MAJOR PROBLEM ANO SOLUTION  AREAS,
 PLUS MODIFICATIONS IMPLEMENTED TO  THE SYSTEM ARE  HIGHLIGHTED BELOW IN THE SYSTEM PERFORMANCE TABLE.


                                          OPERATING  HISTORY
         OPERATION HOURS
 MONTH   BOILER   FGD  SYSTEM   OPERABILITY  (X)
 THE  SYSTEM  WAS  RESTARTED AND PARTICULATE TESTS WERE  CONDUCTED IN  MAY.  THE SYSTEM WAS SHUT  DOWN  DUE
 TO PLUGGED  CHEMICAL  FEED LINE TO THE CLARIFIER AFTER RESTART.  AROUND JUNE 10, THE SYSTEM WAS
 SHUTDOWN BECAUSE  OF  SIMILAR  PLUGGING IN  ANOTHER PART OT THE  LINE.   THE  UNIT RAN FOR  ABOUT TWU WEEKS
 IN JUNE.

 THE  FGO SYSTEM  WAS DOWN  IN JULY AND  AUGUST FOR REPLACEMENT OF  GRAVITY FLOW LINE  WITH  AN  OPEN FLUME.
 OCT.  75   2331     1848         79

 THE  FGU SYSTEM  RESTARTED ON  SEPTEMBER 8,  AND OPERATED DURING  THIS PERIOD  AT AN AVAILABILITY  FACTOR
 OF 80 PERCENT.  THE FIGURES  GIVEN FOR UCT08ER REPRESENT  THE  OPERATION HOURS FROM  SEPTEMBER 8 TO
 NOVEMBER 9.
 DEC.   75   2135     U50          59

 THE FGO SYSTEM OPERATED WELL DURING  THE REPORT PERIOD EXCEPT FOR A  SCHEDULED HOLIDAY  SHUTDOWN FROM
OECEMflER 23 TO JANUARY a, 1976.  BECAUSE OF PROBLEMS WITH SOLIDS AND SOLIDS CARRY-OVER,  G.M. CON-
DUCTED STREAM TESTS DURING  DECEMBER TO DETERMINE  WHETHER THE CARRY-OVER OF SOLIDS WAS DUE TO A HIGH
                                                50

-------
                                                                                    STATUS  AS  OF  07/30/7*1
                                       SECIlOiv  9  (Cl)iiU'JUF.i))
                PEHFliRMANCt  UESCKTHTJON FUK DPL •< ^ T I.J'« * L  KGi;  SY.ittu5i uN INDUSTRIAL MUlLt^b
GENFKAL MOTDHS CllHPOKATIUN;  PArtMA,  (JHtl) ( C ON T I r.ltt !'l )

        OPERATION HOURS
MONTH   rifULER  FGIJ  SYSTEM   UPLRAHILITY 1%)
SOLIDS RECIRtULATIUN RATe.   Irit Mil) SYSTL"' AAS DurtN  HOST  OF  DELFMER BECAhSF OF  IHtSfc  TESTS,  ftHlCH
CAUSED TriF LOW UPERABILITY  FACTOR.
Ffc'tf. 76   .£9^7      119f>           10
G.M. HAS FOUND SOLIDS  CONCtMT RA TI On IN THh Cl.AklFItW TOO HIGH K1K t'FFICTtNT SYSTEM  ORF.K Al ION.  A.D.
LITTLE INAS SCHEDULED TO  CO'MOOCI TESTS OM  THE S»Sie*t  IN  APKJL AS PAfi T Or Ai\ FHA  EVALUATION PKUGHAK).
hAH. 7fa   U79       dH(l            /
APK. 76   10««       tt«7           78
THt LOrt UPE«ABIL1TY  INDEX  OUklNG THE MONTH n^ NArtCh  nESULTtD FKUM EXTENSIVE MODIF 1C AT IONS PEhFORtoFl)
ON THF SYSTEM bY  6.M.  OOWTNG THIS  PERIOD  THE SLMOH6FK 6Lu«HuOwN Ai\iO  SCrtOUciEK FLOW lull) ICAT ION SYSTEM
rtAS hEVISEO.  FHOM  APRIL 11 10 THE  t.MD OF  I Ht MOi\,Tn  1 HE  SYSTtM fliAS  OPtHAdLt 100%.   OURlfiG THIS
PEWIOO ALL SYSTEM MODIFICATIONS WEKt COMPLETED AiMD ALL  MAJOR PK08LEM ArtEAS CuRSECTED.
MAY  76   Ua9      lu«£           91
JUIM. 7o    9
-------
                                                                                      STATOS A3 UF 07/30/76
                                         SECT KIN  9 (Cni'iTIMuPo)
                  HFKFURMANCE DESCRIPTION  Km  UPt k«T l,l,-.«L FG,, SYSTEMS ON  INDUSTRIAL  BOILERS
 GFivEKAL  MlirOKS CORPORATION; HAKMA, (JHlu  ICON I IhillEO)

          OPERATION HOUWb
 MUivTM    uCHLER  FGO SYbTEM  UPLHABILITY  U)
      REPLACEMENT OF Ut.MISTfcR PADS.
      AliUATOH  PROBLEMS.

 • HE SYSTEM  WAS RETURNS ,0 SERVICE THE SECOND  KFEK  ,N  OCI03ER.  F«0 BORERS AND  THEIR  CORRESPONDING
 .CK.mHtKS -EKE PUT  BACK IN tHF. GAS STREAM.   PRu^MS  ENCUUNTtRED STEMMED PRIMARILY  FROM  A MECHANICAL
 COLLECTOR MALFUNCTIONING HtSoLIINS IN EXCESSIVE  PARTICULATt LOADING IN THE MODULES  ANO EVENTUALLY
 LAuSINb  WIDESPREAD  PL.lbGINU UF Ht LO.ER BUBBLE-CAPt TRAYS.   SHUTDOWN AND CLEANOUI OF MODULES  PLUS
 rtfcHAlKS  TO  THE MtCHANJCAL  COLLECTOR WERE REUUIKED.  SYSTEM  RES.ART OCCURRED NOVEMBER 8.
 «AJOK HOtllFICATIONb FFRFORMEU  TO ThF  DOUBLE  ALKALI SYSrFM DUKlNG THE PERIOD INCLUDED THE  INSTAL-
 LATION OF A GREAT LAKES PH MONITOR AND CONTROL UNIT FOR  THE  REGULATTUN OF LIME FEED TO THE  RE6EN-
 NATION REAC10R-CLAR1FIER  UNIT.   THIS UNIT EMPLOYS A DIGITAL  READOUT AND HAS SCHEDULED FOR  OPERATION
 SUhETI*E IN NOVEMBER.   SUPERIOR  CRYSTAL GROWTH OF THE  CALCIUM  SULFITE/SULFATE SALTS RESULTED  BY
 KiMNINtt A SEEDING LINF  SACK  TO THE RfcAC TOR-CLARIFIER UNIT.
 NOV.  76   13dl       787           60
 uFC.  To   I5b<)       i4<»           ?_£

 OUKING  THE LATTER PART  OF  NOVEMBER ANO EARLY  DtCEMaER, THE SCRUBBERS .ERE TAKEN OUT OF THE FLUE GAS
 PATH  BECAUSE OF CONTINUED  SOLIDS  BUTLDUP  IN THE MU  rA«K.   IN  ADDITION.  SOME  PIPING ARRANGEMENTS
 -EKE  MU()IFIED AND 1  Ht oEAR REDUCER IN THE HlX TANK HAD TU UE RtPLACED.   THE  FBI) FIGURES REPORTED  FOR
 THt HO«TH UF DtCtMbEK ARE  NO,  FULLY HEHREStNT AT IVE BECAUSE IT  IS PART  OF  THE  LOCAL  UA* CONTRACT THAT
 ONLY  t,A«  PtRSONNtL CAN OPERATE THE FGD SYSTEM ANu mt»tFuRE THE  SCRUBBERS COULD NOT  BE OPERATED.
 JAN.  77    18!>a      oOB           3^
 FEB.  77    1462      ac<<;           bl

 THEHt. «AS A  FAILURE  UF THE AGITATORS  AT THE MIX TAUKS.   THEY WtRE  LATER REPLACED  WITH  NEW ONES.
 fMt PLAN!  «AS  SHUTOOWN FOR SOME PEKTOl)  DUE  To CUTBACK  UF NATURAL GAS SUPPLY ANO REQUEST  TO CURTAIL
 fcLECl^ICAL CuNbUMPTIUhl.
 APK.  7V    13(JO      11 SB           89
 "•'AY   II    I'ZtZ      Hlo           q£
 bl'ILtC  HUUKS WfcRt LOt, UUt TO LUHER I.UAU IN SUMMER.
 JU'>l. 77    1180     1'lOi          <)U
 JI'L. 77    7(lg       
-------
                                                                                     STATUS  A3 OF 07/50/70

                                       SECT JON  "J  (CO'iT INuEO)
                         'JCE  DESCRIPTION r()R U P t * A T 1 ON 4 L  VGD bY.SItMS DM INDUSTRIAL  rtUlLtRS
I:,H.FK<\L .-minus CURPOKA MUM;  PAKMA,  I.IMIU ICUNI livjtD)

        OPfc WAT 10.-1  HOURS)
t-iduTri   (JlHLtP   KJO  SYSTtM  OPERABU1TY U)
UtlrlNK  THIS  LOW-LOAD PtRIOO  THt LlMt FEED HUMP  A,Ml) LIME  FEED LINtS WbRE  CLEANF.J.   GENERALLY, EVEHY
3IJI-MLK  A,M  ANiMUAL Ft,D Ol/Et
-------
                                                                                     STATUS AS OF 07/30/7B
                                        SECTION  9 (CONTINUED)
                 PERFURMANCE  DESCRIPTION FUR OPERATIONAL FGO SYbTEMS UN  INDUSTRIAL  BOILERS
   INSTALLATION NAMt
   INSTALLATION LOCATION
   SOURCE CHARACTERISTICS

   SOURCE RATING
   NUMBER OF SEPARATE FGO UNITS
   SOURCE CAPACITY
   CONTROL SYSTEM VENDOR
   COinTKOL PROCESS
   NErt  /  RETROFIT
   START-HIP DATE

   CONTROL SYSTEM STATUS
   S02  EFFICIENCY
   PARTICIPATE  EFFICIENCY
   nATER  MAKE-UP
   SLUDGE OR BY-PRODUCT  DISPOSAL

   CONTROL SYSTEM COST
 GENERAL MUTORS CuRPORATION
 ^ONTIAC,  MICHIGAN
 COAL  (O.B1X SULFUR)
 ALSO  WUUD,  PAPER,  AND CARDBOARD.
 107.300.SCFM (TOIAL  - 2 BOILERS)
 350,000 LB/HR  STEAM  (TOTAL - 2 HOILERS).
 LB/HR  i>T£AM (TOTAL  - g BUlLtRS)
 2
 VO M«v  (EUUH/AI.ENT) ;  TOTAL - a BOILtRS
 PEA800Y ENGIiMFtRING
 SOOIuM  HYDRUXIuE  SCRUBBING
 NEn
 APRIL,  197b
 bYSTLM  OPExAFEu TWU  MONTHS IN EARLY 1973.
 UPERATIUNAL
 NOT DETERMlNtD
 65X
 UPtN LUOP;  50 iiPM
 DErtATEKEO SLURRY Tu  LANDFILL
 5X  SuLins SLURRY DEWATtRtD AND  TU .L-AUOFILL
CAPITAL: SbOo,uoo imra).   THIS is  THE"-TOTAL
 INSTALLED COST.
                                        BACKGROUND INFORMATION
    1HE GENERAL.  MOTORS  TRUCKS  AND  COACH PLANT LOCAIED AT PONTIC, MICHIGAN  OPERATES TnO BOILERS TU
GENERAIE STEAM FUR  PROCESS  REQUIREMENTS. BuILEh ,MO. b, INSTALLtD IN  1972 BY  ERIE  CITY, 13 RATED AT
186 «l" HTU/HR UR  IbO.OuO  LBS/HK  uF  STEAM. tJOILtR NO. 8, INSTALLED IN  197d  BY  RILtY,  IS RATED A! 250
MM Htll/Hrt OR200.000 LHS/HR  OF  STtAM.   THt 1-UbL USEu IS CUALtu.Ol X SULFUR),  AMD  SULID  KE"KUSE (PAPER
ANu CARDBOARD).   THE  PAR TICULA I E EMISSIONS ARE CUNTRULLElJ BY MLCHA.MICAu COLLECIORS SUPPLIED BY ZuRIV
INOUSTKlcS, DESIGNED  Tu UPtRAlh  AT  93  * EFFUItNu Y, nlTri A PRtSSURE  DROP  OF  ABOUT  3  IN.  KIG.
  PF.AHUDY ENGINEERING SUPPLIED Two  *ET  SCRUBBERS IN APRTL 1976, PRIMARILY  FOR  ADO I T IUNAL  PARUCULA1E
CONTKOL.  tACH SCRURbEKC  Id  FEET DIA.X  21. 5  FELT  HIGH) CONTAINS 5 IMP I NGF .IE-NT TRAYS  AND  OPERATES
rillH A L/6 OF b GAL/lOud  «LF .   I HE SCwimntR EFFLUtNT IS MIXED 1 1 T H CAUSTIC  AND MAKEUP «ATER IN A
 HUL.J 1 AUK, AND PUHPLO  TU A  CLARIFIFK.  THE UVFRF(.UA IS RECYCLED TO THE SCRUBBER,  THUS  SIGNIFICANT
SO 2 CONTROL IS -ACHIEVtO.  THE UNDERFLDw  IS SEnjT Tj A ,,ASTc I RL A T F.,1ENT  PLA.MT,  AHERE  I HE  FLYASH IS RE-
MOvhu AMU LANDFILLED. THE EFFLUEiMT  0 1 SC H A Wbt "FKOM IHt rtASTt TRtATMENT PLANT  IS 10-23 GPM.

-------
                                                                                       3TAIUS A3 UF
                 PEKKui'MAfJCt  DFSCKHMUH Fl)K UHc H A F I U.iHL Hii) aYjltMS UN I,«UUSI«IAL  l




t-El^FRAL rtOTOKS  C URPUK A'l I U'M ;  POiMTlAC, MICHIGAN  ICu.'-f I I rtllcl) )






    THE SCKUd8ERS»  THAYSr  AMD  MlaT r u TM TM IOKS I  ^<«jIAL VANt FYHF)  A^h ALL MADE  UK  31bL SS.






                                           DPEKA I I.Vli  H1S1 (IKY




2ND UIIARTEH-19/b    IliMSIAULt  PH CUMlKuL AND  rttAh  nP  WLCHAi\IICAL  tUUlPEwENr HANliLINU  IHt I-LTASH  SLURRY




WE«E MAJOR  STARTUP PirOtlLEMS.




3i

  • -------
                                                                                         STATUS AS OF 07/30/70
                                            SECTION  
    -------
                                                                                       bTATUS AS UF 07/3U/78
    
    
    
    
    
    
                                          SECTION  9  (COiMT 1-NUED)
    
    
    
    
                                JESCHTKUdN I-OK OPERATIONAL  FGU  SYSTEMS  UN INDUSTRIAL BOILERS
      l!i,->TALLATUIN  NAMt
    
    
    
    
      INbT AULATIuN  LUCAT1DN
    
    
    
    
      b-ilURLr  CHARACTERISTICS
    
    
    
    
      SOURCE  RATING
             OH  SEPARATE F60 UNITS
    
    
    
    
           E  CAPACITY
    
    
    
    
      CONTROL SYSTEM VENDOR
    
    
    
    
      LOlvTRDL PROCESS
    
    
    
    
      HF.V  / RETROFIT
    
    
    
    
      START-UP DATE
    
    
    
    
      CONTROL SYSTEM STATUS
    
    
    
    
      SOd  EFFICIENCY
    
    
    
    
      PART1CULATE EFFICIENCY
    
    
    
    
      rtAIFK MAKE-UP
    
    
    
    
      SLUDGE OR BY-PRODUCT DISPOSAL
      COmT-ROL SYSTEM CUST
    GENERAL MOTORS CORPORATION
    
    
    
    
    TUNOAA,\DA, .\t>\ YufiR
    
    
    
    
    COAL (1.2X SUI.FllK)
    
    
    
    
    4i?,()UO SCF'1  CTUTAL -  4  BUTLEHS)
    
    
    
    
    36,000 ACFM  a «0fa F,  FJR  EACH OF 3 FGD SYSTEMS
    
    
    
    
    ^9,600 ACFM  ol iSO F,  FOR  1  FGD SYSTEM
    
    
    
    
    jau.uOU L8/HW bTEAM  (TOTAL  - t BOILEKS)
    
    
    
    
     a
    
    
    
    
    65 MW  (EQUIVALENT);  TOTAL - 4 dOILERS
    
    
    
    
    FMC ENVlKOivlMENTAL EQUIPMENT
    
    
    
    
    bODIUM HYDROXIDE  SCRUBBING
    
    
    
    
    WETRUFIT
    
    
    
    
    JUNE,  1975
    
    
    
    
    OPERATIONAL
    
    
    
    
    90X-V5X  (1,000  PPM  S INLETJ
    
    
    
    
    *OJt  11.0  LU/HM  8TU  AT INLET)
    
    
    
    
    OPEN LUOP
    
    
    
    
    OEnATEriEU SLURKY  TO  LANDFILL
    
    
    
    
    FLY  ASH  AND  NA£SU3/S01 WASTE LIUUOrt DEWATEKED  AND  THEN TO
    
    
    
    
    SAUITArtY  LANOFILL
    
    
    
    
    CAPITAL:  $^,aoo,ooo   ti97t)
                                                       INFORMATION
    
    
    
    
        THE CHEVROLET DIVISION  OF  GENERAL MOTORS HAS A MOTOR PROUOUTION  PLANT  AT  TONAWANUA, NEH YORK.
    
    
    
    
          ARE i cuAL-Fiwbo BOILERS AT  THE FACILITY WHICH RUKN  1.16 PERCENT  SULFUR COAL WITH A HEATING
    
    
    
    
    VALUt OF la,b50 HTU/L'a.   TUP  TOTAL  COAL FfctD RAtt IS 17  TONS/HH  WHICH  IS  F.UUIVALENT TO «12 MM BTU/HR
    
    
    
    
    UF htAf INPUT U«  540,DUO  LoS/HR  uF  STEAM.  THE HUILERS ARE RATED  AT  A  TOTAL OF 3£ MW.
    
    
    
    
        uwt SCRUDStR  HANULtS  3^,000  ACFM AT 350 t- wHERtAS EACH OF  I HE  OTHER THREE 36,000 ACFM AT aub F.
    
    
    
    
    IHLHE IS A CYCunNE btFuPE ANU  AFIF.K SCRIIBHtR FuR MUST COLLECTION  AND MIST  REMOVAL PURPOSES, RESPEC-
    
    
    
    
    TIvELY.  THF VARIAbLt  InROAT  VENTURI SCHOBriERS WERt SUHPLltO BY  FMC  CORP.   ThE PH OF RECYCLE
    
    
    
    
    SCRilniiLH LIQUOR  IS CuNTRULLED  AT  7.0 Ami) A L/S RATIO OF  dO GALLONS/1UOU ACF IS USED.  PRESSURE DROP
    
    
    
    
    ACrtMbS FACH SCWDBHER  IS  10  TIM. /Iti.   CAOSTIC bOUA IS ADOEU  TO THE  SPENT  LIQUOR IN A SEPARATE RECYCLE
    
    
    
    
    I AUK.  THE BLEED  OFF  RATE FROM THF  RECYCLE TAN* VARIES FROM 25 -  100 GP^.   THE DISCHARGE CONTAINS
    
    
    
    
    H. YASH AMD SODIUM SOLFATt.   THE  FI.YASH IS CONTROLLtO AT  LESS THAN  U SUSPENDED SuLlDS.  THE EFFLUENT
    
    
    
    
    is DISCHARGED TO  THE  /VASTE  TKEAT.»IF.NT PLAI\T AFTER AERATUM.  THL  AVERAGE INLET CONCENTRATIONS ARE
    
    
    
    
    u.OI l.n/MM 13TO UF SUt  AND  1 L8/MM  nTu OF PARTICULATE.  ThE EFFICIENCY  OF  S02 REMOVAL IS 90« WHEREAS
    
    
    
    
    IriAT ill- FARTICllLATt  KKl-UWAL IS 8UX-9aX.
    

    -------
                                                                                        STATUS  AS  OF  U7/30/78
    
    
    
                                           SFCTIOn  9 (CONTINUED)
    
    
    
    
                     PERFORMANCE  DESCRIPTION FOK OPERATIONAL FGU SYSTEMS UN INDUSTRIAL  BORERS
    
    
    
     GENERAL  MOTORS  CORPORA I ION;  IONOWANOA,  NEW Yu*K (CONTINUED)
    
    
    
    
    
    
    
         EACH  SCRUBBER  AND  THE  CYCLONIC  OEMISTEK IS MADE UF 316L SS.  PLUME REHEAT IS NUT INCORPORATED
    
    
    
    
     IN  THE SYSTEM.   THE  ENERGY HEQUIREME*TS FOR THE SYSTEM ARE  ABOUT 3 - 5 * OF THE FoEL aURNED.
    
    
    
    
    
    
    
    
    
                                              OPERATING  HISTORY
    
    
    
    
     3RU  ULIARTERM977     AVERAGE  OPERABILITY OUKlNS TnlS PERIOD WAS REPORTED TO BE 10UX.
    
    
    
    
     1TH  UUARTER-1977     MAJOR  PROBLEMS  HAVE dEEN  PH CONTROL ANO RECYCLE PIPE  EROSION.  CONTROL
    
    
    
    
     SENSORS/MODULATING MIXER VALVE  REPLACED FON PH CONTROL AND CAST IRON PIPE «A5 USED TO
    
    
    
    
     REPLACE SS RECYCLE PIPING.   DURING  NOV  -  DEC  CONDENSATION  FOLLOWING THE OEMIbTER
    
    
    
    
     HAS  CORRODED THE STACK LINING.   A DECISION  HAS BEEN MAOF  TO RELlNE  THE STACK.
    
    
    
    
     1ST  dUARTER-1978     THt STACK, rtAb ,\or RELlNEO.
    
    
    
    
    
    ^NU  UI.ARTER-197»     ONE MORE CYCLONE WILL BE  RETROFITTED AFTER EACH BOILER IN ORDER 10  REDUCE THE
    
    
    
    PAKTICULATt LOADING  TO THE SCRUflriERS.
    

    -------
                                                                                        STATUS  « J  UF  U7/30/76
                                           bf-CTlOivl  ° ( !.(>.•-! T I Will- u)
    
    
    
    
    
                    PERFORMANCE  I'JF.SCRIPT lOiv FM* uPr..n AT I'1n«L KJ\I  SYSTEMS  ili\, IMJUSIRIAL
      INSTALLATION NAMt
    
    
    
    
      INSTALLATION LOCATION
    
    
    
    
      SOURCE CHARACTERISTICS
    
    
    
    
      SOURCE RATING
    
    
    
    
      NUMBER OF SEPARATE FGO  UNITS
    
    
    
    
      SOURCE CAPACITY
    
    
    
    
      CONTROL SYSTtM VENDOR
    
    
    
    
      CONTROL PROCESS
    
    
    
    
      NEW / rtF.IROFIT
    
    
    
    
      START-UP DATE
    
    
    
    
      CONTROL SYSTtM STATUS
    
    
    
    
      802 EFFICIENCY
    
    
    
    
      PARTICULAR EFFICIENCY
    
    
    
    
      WATER MAKE-UP
    
    
    
    
    
    
    
    
      SLUnSE OR BY-PRODUCT  DISPOSAL
    
    
    
    
      CONTROL SYSTEM COST
    l,FuRt.I A-PALlF 1C  PAPE«  CO.
    
    
    
    
    !, K u b 3 E I T i AKl\AnSAS
    
    
    
    
    L-,Ar
    -------
                                                                                          STATUS  AS  OF  07/30/78
    
    
    
                                             SECTION  9 (CDriT 1MUEU)
    
    
    
    
    
                      PERFORMANCE UESCrfrPTIO',.  K)K  uPEKATIUNAL HGu SYSTEMS  ON  INDUSTRIAL BORERS
       INSTALLATION  NAME
    
    
    
    
       INSTALLATION  LOCATION
    
    
    
    
       S'luRLE CHARACTERISTICS
    
    
    
    
       d'liiKCe RATING
    
    
    
    
       MjMrttrt OF SEPARAIE  FliO UNITS
    
    
    
    
       SHuWCE CAPACITr
    
    
    
    
       LG.Ui?<)L SYSTEM  VENDOR
    
    
    
    
       UONTKOL PRUCcSS
    
    
    
    
       nlErt / rJFlROFIT
    
    
    
    
       STAk'T-UP DATE
    
    
    
    
       CONTROL SYSTEM  STATUS
    
    
    
    
       SOU EFFICIENCY
    
    
    
    
       SLUDGE nw BY-PRODUCT  DISPOSAL
               SYSTEM COST
     GETTr  ulL COMPANY
    
    
    
    
     IJAKF.RSl-" ItLO.  CALIFORNIA
    
    
    
    
     COAL  (1.1% SULHUiV)
    
    
    
    
     '2,000  SLFM (TOTAL - 6 BUTLERS)
    
    
    
      1
    
    
    
    
     30  MA  (EQUIVALENT); t> BOILtRS,  EACH  a) 50 MM 6TU/HR.
    
    
    
     FMC tNVlKONHENIAL EOUIHMEMT
    
    
    
    
     SOOIUM  CARUO.MATE SCRUBBING
    
    
    
    
     hETROFIT
    
    
    
    
     JUNE,  11n
    
    
    
    
     UPtRATiONAu
    
    
    
    
     90 + X  (600  PPM  al  INLET)
    
    
    
    
     HOLOIN6 PONO FOR EVAPOKATION
    
    
    
    
     10 GPM BLEEDOFF  TO A BLOHOOrtlM TANK.   THE SLOWDOWN IS THEN
    
    
    
    
     SENT Tu A  DISPOSAL POiMD ONCE A WEEK.
    
    
    
    
    CAPITAL: $aoo,ooo  (1977).  THIS COST  INCLUDES  THE ABSORBER
    
    
    
    
    MUOHLE, SODA ASH TANK,  PUMPS, ANO PIPING.   IT  DOES NOT
    
    
    
    
     INCLUDE THE STAC*,  DUCTING,  ENGINEERING.  OR  OVERHEADS.
                                                OPERATING: «59o,ooo/YR  lot 510 OAYS/YW).   THIS  COST  is
    
    
    
    
                                                EQUIVALENT Tu iO.lb/NM  Bill ANO HMCLUuES  THE COST  FOR
    
    
    
    
                                                SODA ASH, ELECTRICITY,  AND SCRUBBER MAINTENANCE.
    
    
    
    
    
    
    
    
    
                                             BACKGROUND INFORMATION
    
    
    
    
        >,ETTY  OIL  COMPANY HAS AN OIL SITE  NEAR 8 AKE «SF i ELD, CALIFORNIA  WHICH OCCUPIES ABOUT  15  SQUARE
    
    
    
    
    MILES.   THERE  ARE t 3b STEAM GENERATORS;  100 AllH A HtAT rtATE OF 50  MM BTU/riR AND 36 WITH A  HEAT
    
    
    
    
    *ATfc OK  dO  MM  bTo/.IR.  THE FuEL USED  IS  CRUDE OIL WITH l.U SULFuR  AND A HEATI.MG VALUE OF 6.4 MM
    
    
    
    
    rtTu/bBL.   STEAM IS DISTRIBUTED THRUIIGHUlll  I HE OIL FIELD BY INSULATED PIPELINES;  ANO INJECTED  INTO
    
    
    
    
    lilt ulu  «ELLS.   LONOLNbAIIuN Oh IHt STEAM  KEoUCES I ML VFSCJSIH OF  THE OIL,  WHICH FLOWS FREELY  TO
    
    
    
    
    Iht S'lKFACE  ALONG WITH THE «AT(;R.  THE  OIL  IS SEPARA.EO FROM WATER  BY OECANTATION IN SETTLING TANKS,
    
    
    
    A'H) KlIRlHtD BY  DISTILLATION IF REUIUREO.
    
    
    
    
    
        IHc  rLUE GAStS (150,000 ACFM fl 500  f)  FROM SIX LARGE BOILERS  (50 MM BTU/HK)  ARE MANIFOLDED
    
    
    
    
    IMO A TRAY  ABaORHtR  (13.5 FEET DIA A  55 FEET HIGH)  AHICH rtA3. RETROFITTED  IN JUNE 1977 BY FMC,
    
    
    
    
    Lf.VlKt.'.riLNIAL  EliUlPMtNi  DIVISION.  THE  PRJLHSS USE,;  IS  SoDiUM CARBONATE SCRUBBING.   THE LUUOR  IS
    
    
    
    
    .•lAiMAi,.tD  Al  A  PH Ol-  b.», AND REC IRCIJL A T ED  ,V I] H  A I./G  RATIO Of  b. 
    -------
                                                                                         STATUS  AS Of 07/i()/7B
    
    
    
    
    
                                            SFCTIOlM   9 (CU.JT J.XJFM)
    
    
    
    
                     PfKFuRMANCt DESCRIPTION  t-0*  uPt X AT I [j.\, AL FUO  SYbTt^S  ON IM'JSTHIAL BOILERS
    
    
    
    
    IJMTY J!L COMPANY;  *AH  AiMO LtVtL CONTROLLFwS.
    
    
    
    
    
    
    
    4Th i,'!.IAKIEK-1977   TtiF. FAN ROToR  *AS S T Rt NliT HEnEu  AiviO CLEANED JF THE  SCALES.   THE FAiM BEARING  BURNED
    
    
    
    
    UP.   II WAS  REPLACED AND  THE FAN  WAS REALIGNED.
    
    
    
    
    
    
    1SI uli«KIEk-197»    HlbH  SIACK  DISCHARGE VtLUCITY  ihO FPS) CAOb.FO BY  SMALL  STACK  DIAMETER; AND POOR
    
    
    
    
    LUCA1IO-J  OF  MIST ELIMNATOK Cl 00  CLOSE To  bTACK  TRAMSIIION SECTION) RESULTED  IN HIbH ENTRAINMENT  OF
    
    
    
    
    URUPLFfS.  THF STACK Awn  TOP SECTTUM 01-  I'Ht SCRUrilttH WERE  REDESIGNED.
    
    
    
    
    
    
    c!'Mli  UIIARTFR-197U    THt MESH OLMISTEn ftILL  BE  REPLACED  BY  A MUUTEHS CHEVERON  TYPE MIST ELIMINATOR.
    
    
    
    
    A  MiLM  F-LFXITRAY WILL  BE  INSTALLED  AoOvf THF PK£bEi\lT 3RD  TKAY IN JKDtR Tu IMPROVE S0£ REMOVAL
    
    
    
    
    tF-r TCItA-'CY,  PAKilCOLARLY  DURING IiJKNuOnN CoNIjTIIuNS.  IHt PH PROBES ARE  FOOLED FREljUENILV.  SEVERAL
    
    
    
    
     lYpfc  OF CONTROLLERS ARr.  PWtStNtLY tiUNi, IFSTtD  FOR HIGH  RELIABILITY.   THE MlLO STEEL REC I HCUt AI ION
    
    
    
    
    LliMFb rtFKE  EKOuEU,  AND  WILL BE  RtPLALFu oY  31hL SS.   THE  AIR BUBBLtR  IN  SOOA  ASH TANK LEVEL
    
    
    
    
    CdiMlKOLLtK   IS OFIEN PLOGUEl).   IT  ill U L BF. RtPLACEO BY A  DIAPHRAGM  TYPt  LEVEL CONTROL DEVICE.   THE
    
    
    
    
    ril. urti;0,i|i-'  TANK OUTLET LINE  nAj  OEVELOPEO SCALING.   A  POSITIVE DISPLACEMENT PUMP WILL 8E INSTALLED  IN
    
    
    
    
     MIS  I. IVt,  AND  flN !NhIBITO« MAY UE  AlJDtH IN THt I ANK LIOUOK.
                                                       bl
    

    -------
                                                                                        STATUS  AS  OF  07/30/70
                                            SECTION  9 (CONTINUED)
                     PERFORMANCE  DESCRIPTION  FOR  OPERATIONAL EGu SYSTEMS UN .INDUSTRIAL BOILERS
       INSTALLATION NAMt
       INSTALLATION LOCATION
       SOURCE CHARACTERISTICS
       SOURCE RATING
       HllMHEW OF SEPARATE FGD UNITS
       SOURCE CAPACITY
       CONTROL SYSTEM VENDOR
       CONTROL PROCESS
       NF.w / RETROFIT
       START-UP DATE
       CONTROL SYSTEM S1AT.I.IS
       S0£ EFFICIENCY
       PART1CULATE  EFFICIfcMCY
       rtATER MAKE-UP
       SLUDGE" OR BY-PROOUCT  DISPOSAL
    
       CC/NTROL SYSTEM CUST
     GREAT  SOUTHERN  PAPER CU.
     CEOAR  SPRINGS,  GEORGIA
     tiARK AND  CuAL UR  OIL C1.OX-2.0* SULFUR)
     420,bOu SCEM  (TOTAL  - i  BOILERS)
     S
     100 MW  (EQUIVALENT); TOTAL  - 2 TOILERS
     AIRPUL  INDUSTRIES
     CAUSI1C AA3TE STREAM
     RETROFIT
     1975
     UPERATIONAL
     85Jt-^Oi! (1,000  PPM AT  INLET)
     99.1%  (DESIGN:  a.5 GR/SCF AT  INLETJ
     UPEN LOOP; 3iO  - auO  GPM PEK  AriSuRdER
     rtASTErtATER TKEATilENT  AND DISCHARGE  Tu  KlVER
    CLARIFICATION FOLLOWED 8Y PONDING ANO  DISCHARGE TO RIVER
    CAPITAL: sooo.ooo (1974).   THIS is  THE  EQUIPMENT  CUST FOR
     THE TWO SCRUBBER MODULES.
                                            UACKGKOUNu INKOKMATION
          THE  FGD  SYSTEM  AT  GREAT  SOUTHERN PAPER AT CtOAR SPRINGS, GEORGIA CONSISTS  OF  TWO  AIRPOL  SODIUM
    SCRUBBING -TRAINS  CONTROLLING  EMISSIONS FROM I Wu COAL-FIRED BUI|_ERS, EACH RATED  AT  50 Mw
    (EUUIVALENT)  AND  EACH PROOUCINb  bOO.OOO LB/HR  STEAM.  THE FUELS f IREU IN THE 80ILEHS TYPICALLY  HAVE
    THE FOLLOWING  SULFUR CONTENTS: CUAL  - l.b% ,  OIL - 1.5*. AND BARK - d.0%.
          THE  STAINLFSS STEEL  SCRUBbERS  HANDLE  A COMBINED TuTAL OF VOO.OOO ACFM AT 42b  DEGREES  F.   THE
    PRESSURE  DROP  ACROSS A  SCRUrtilER  IS  AHPROX IM A TEL Y 7 INCHES rt.G. WITH db To 90% SULFUR DIOXIDE
    REMOVAL EFFICIENCY.  THE  SULFUR  CONC t N T R AT I ON  OF THE FLUE bAS IS 1000-1200 PrK  A^D-THE PARIICULATE
    LOAD ING IS 4.5 GR/SCFD.
          THE  SCRUBBER UNDERFLOW IS CUMPOSEO  OF FLYASH ANu SODIUM SULF I r E/ SULM TE SoLUTIUN.   SOLIDS
    CONTENT tFLYASH)  IS  IYPICALLY i  TO  S  X BY  HEIGHT.  SCRuBdE'R WASTE «ATEK fllfH AN AVERAGE  PH  OF  4.5
    IS PuMOEU ANO CLARIFIED WATER IS  RETURNED  TO  THE RIVER.
                                              OPERATING  HISTORY
    •4TH IJIIARIFH-1977    THE EXPANSION  JOINT  6F.lrtc.KN  1 HE EXISTING STACK AND SCRUHrtER HAD TO HE REPLACED
    IN SEPIFMBtK.  SOME iNIE'RNAL WEAR  ,-, A S UFltCItO On  I Mr.  PMMPo DUE  TO TnE ASH CUMTEivT.
    ERUSKMv ANU PLUGGAGE PROBLEMS rtlTH THE PH HROBhS  HAVE  BHEN  ENC UJN T t RED .   THE PLANT WAS IN
    THt PROCESS OF CHANGING IHE CONTROL PH AND  MUVING  THE  PKOBES.   IAMKS AMD NECESSARY
    

    -------
                                                                                              STATUS  AS  JF U7/JO/7S
    
    
    
    
    
                                              SECTION  ft HH T I ll.J AL hRu  SYi'L-tS ON  IM1USIW1AL
    
    
    
    
    bHtAT  SOUTHERN PAPfH  CO.; tl-liAK  bPi
    -------
                                                                                             STATUS  AS OF  07/30/78
                    HF.kFllR.'IAnCt UE.j
    
    
    
    
    
    
    
    
     l'Jbl ALLA I IljN  NAMt
    
    
    
    
     IMSTALl-ATIliN  LOCATION
    
    
    
    
     £>oi)f.R  TREATMENT  AND DISCHARGE TO  RIVER
    

    -------
                                                                                         STATUS AS OF  0?/Ji)/7S
                           ShCTlON  9  ICHitTINUFl))
    
    
    
    
    
    PERFORMANCE DESCRIPTION FOR OPERATIONAL  FRiJ  SYiiTtMS
                                                                              I'JDUS|RI»L TOILERS
      INhTAI LAI IUN NAMt
    
    
    
    
      Pi.STALi.AT ION LuCATl(nX  thua PPM  n)  INLLT)
    
    
    
    
                               90X
    
    
    
    
                               «ASTt«ATtR  TREATMENT AND DISCHARGE  TO CIIY SEWER
    
    
    
    
                               bLtEu-UFF STKEAM TO HOLDING TANK
    
    
    
    
                               CAPITAL: $^2.4,000 (tvr.4).  THIS is  THE  TOTAL INSTALLED COST
    
    
    
    
                               OF THE FbD  SYSTEM.
                                               OPERATING:  sio,2uo/YK.   THIS  INCLUDES ELECTRICITY.
    
    
    
                                               MAI,\llENt'.Ct, LA8UR, AND  MAIFKTAI.3.
                                            BACKGROUND INhOKMATlOM
    
    
    
    
        THt GREAT •rtESTER^  SUGAR COMPANY HAS  two  COAL-HRtn BUILEKS AT  THE  FIIMDLAY, OHIO PLANT.   EACH
    
    
    
    
    iJfilLtK IS RATFU  AT  bO.OOu LBS/hR nh STtAM;  AND  BURNS COAL rtlTH 1.2  PERCENT AVERAGE SOLFUH,  9.2
    
    
    
    
    PthfENT AVERAGE  ASH,  AND A HEATING VALUE  (IF  1 2 , 7 1 b RTII/Lb.  THE SUGAR  FACTORY IS OPERATIONAL  ONLY
    
    
    
    
    i MONTHS OF EVERY  YEAR,  UURINb THE FALL  UUAKTE'K.
    
    
    
    
       TnF Fi,0 SYS1EM  »iAS  REMOFlTIEl) IN OCT.  19V«  AS A PROPRIETARY DESIGN PRIMARILY FOR PARTICOLATE
    
    
    
    
    Cl.iNlKdL.  THE FLUF  GAStS FROM TWu BdlLtWS  I 1^0,000 ACFM at bib F)  PASS  THROUGH rtUL T ICLONES ,  *i»D  THEN
    
    
    
    
    AWE strrjT THROUGH A  VENIORI SCRUB«EK, WHICH  OHEKAIES WTIH A PRESSURE DROP OF ? IN. OF WG  AND L/G
    
    
    
    
    VALOt 
    -------
                                                                                          STATUS  AS UF 0 I /la/7 a
                                            SFtTIUM   g  (CONTINUED)
                      PERFORMANCE DESCRIPTION FUK OPERATIONAL.  HGU bYSTEMS ON INO.JSIKIAL  HQtLEKS
        INSTALLATION NAME
        INSTALLATION LOCATION
        SOURCE  CHARACTERISTICS
        SOURCE  RATING
       NUMBER OF  SEPARATE  FbD  UNITS
       SOURCE CAPACITY
       CONTROL SYSTEM VENDOR
       CONTROL PROCESS
       •Mfrt / RETROFIT
       START-OP DATE
       CONTROL SYSTEM SI AT US
       S02 EFFICIENCY
       PAKTJCULATE EFFICIENCY
       SLUDGE Ok bY-PROOUCT DISPOSAL
       CONTROL SYSTEM COST
     GREAT  WESTERN SUGAR
     FONT  M,uRGAl\i,  COLORADO
     COAL  (i.c;x SULFUR, AVKRAGEJ
     65,230  SCFM (TUTAL - 2 BUILERSJ
     100,uoo  AChM  EACH nj aoo ^  (TOTAL - a  BOILERS;
     25u,600  LHb/MR STEAM ((OTAL - d UOILERbJ.
      ?
     38fa MM  HTU/HR, 31 MW (cQIJH/ALEI»T; ; TOTAL  -  2  BOILERS
     bRtAT  WFbThRiM SUGA'K"
     A'MMDMA-LAUEN HRuctSb «ATPK
     R'EIKOFll
     OCIObER,'  1^76
     OPERATIONAL
     481 I3ot)-tf00  PPM  a)
     V5% (750 I.BS/Hri
    WASTEWATtR  TKtATMEfJT  AND  DISCHAHbE  TO
    CAPITAL: S7o?,ooo  iis?o.).   THIS is  TOTAL  INSTALLED COST
    OF THE ?UD  SYSIEM*
                                                UPERATlMt,: $8H,200/YK  THIS  INCLUOfiS  ELECTRICITY, STEAM,
                                                MAlNTEUEiMCtv LrtHOR, AMU.. MA TE,R TALS .
                                            fiACKGROUNu  INFORMATION
         THE  GREAT  WESTERN SUK«R COMPANY HAS  Iwu  COAL FIRED BuILEftS AT TH£I« FORT MORGAN,  COLORADO PLANT,
    EACH HUILER  IS HATEU Al  i8si000 LBb/HR OF STfcAM; Am.  BURNS CUAL «ITH 0.5a PERCuNT  AVtRAGt  3ULFUR,
    8.7  PERCENT  AVERAGE ASH,  AND AN AVERAGE HEATING VALUE OF  10,17D dTU/LB.  THE SJG«R  FACIOrfY  IS OPER-
    ATIONAL  ONLY 3 MONTHS, OF  EVERY YEAK, DURING  THE FALL  QUATEK.
         IHt  ,-Gl)  SYSTEM WAS RETROFTTTEO TN Off. '76 AS  A PHOPHIETARr UESiliN PRIMARILY FOR  PARTIC04.ATE
    CONTKOL.   THE  FLUE GASES  FKOM EACH HOILER UOO.fluO ACFn a)  400  (- )  PASS THROUGH ,-IUL T ICLO,.£S,  AM)  THEiM
    Ai?L SfNT THROUGH  A VENIURI  SCRUHBFR, WHICH OPERAIES rtliH A PRESSURE  IJROP OF b IN. OF  *G  ANO  L/G
    VALUt OF » GAL/1000 ACh.   The SC«UbHERb ARE  MlLLO-VtD  RY A  COMMON  VESSEL «H1CH CONTAINS A SlNGLt-
    PASS, THREE. StAGE  CHEVtRON  OEMlSffK.  *ASH WATtR KLOB  ,n TnE  DfcMIstEK IS 120 SHM. nITH A FhtoUtNCY
    OF tb MFNUTES  EVERY 8 HOuRS.  1 HE  PKhSSUKt OhOf ACROSS OtHISTEK IS 0.5 l«.  OF *s.   A  CONSTANT dLtEu-
    UFK STREAM OF  bOU  GPM FROM  EACH  SCRUtiHtR IS  SENT To A  POND, WHICH OVERFLOWS INTO ANOTHER HOLDING
    pown.
        (HE VENTURl SCRUbhER,  [HE  PLUG,  liEMISTfcK VESSEL,  AW. THF.  DtMlSIFK ARE  ALL MAUE OF i t oL SS.
    

    -------
                                                                                      STATUS AS OF U7/30/7B
    
                                          SFCTION   9  (CONTINUED)
                   PERFORMANCE DESCRIPTION  F OK  uPK RA TI O.MAL  KUU  SYbTEMS  UN INDUSTRIAL BOILERS
     INSTALLATION NAME
     INSTALLATION LOCATION
     SOURCE CHAKACTERIST1CS
     SOURCE RATING
     NUMBER  OF  SEPARATE  FGO  UNITS
     SOURCE  CAPACITY
    GRtAI  WfcSTtRm SUbAR
    GF-KlNG, NEoRAStsA
    COAL (l.dX SULKIJR, AVERAGE)
    110,OOU SCFM (TOTAL - 2 BOILERS)
    97,000 ACFM EACH 3 4bO F  (TOTAL -  2  BOILERS)
    205,000 LBS/HR S1EAM  (TOTAL  -  2 BOILERS)
    
     2
    «!Q.5 Mft (TUTAL 1 - 15, 1  - 5.5 BOILER)
    21B MM RTU/HK  (TOTAL), 21 MW (EQUIVALENT);  TOTAL - 2  BUILF.RS
      CONTROL  SYSTEM  VENDOR
      CONTROL  PROCESS
      NEW  /  RETROFIT
      START-OP DATE
      CONTROL  SYSTEM  STATUS
      S02  EFFICIENCY
      SLUDGE OR BY-PRODUCT DISPOSAL
    
    
      CONTROL  SYSTEM  COST
    GREAT WESTERN SUGAR
    AMMONIA-LAOEIM PROCESS HATER
    RETROFIT
    OClOfaEK,  1975
    OPERATIONAL
    70%  IfeOO  PPM o")  INLET)
    WASTEWATER TREATMENT  AND  DISCHARGE Tl) RIVER
    EFFLUENT  TO HOLDING POND
    CAPITAL:  $613,000  cms).  THIS is TUTAL INSTALLED COST
    UF THE  FGD SYSTEM.
                                              OPERATING: i3«,6oo/YK  THIS  INCLUDES  ELECTRICITY,
                                              CiAIMlENENCE, LABOR, AMU MATERIALS.
    
    
                                           BACKGROUND INFORMATION
        THE GREAT WESTERN SUGAR COMPANY HAS TWO COAL FIRED BOILERS AT THEIR  GEN ING, NEBRASKA  PLANT.
    BOILER *i IS RATED AT 150,000 LBS/HR OF STEAM AND WAS SUPPLIED BY ERIE CITY  IN  1963,  WHEREAS BOILEH
    #2 IS RATED AT 55,000 LB/HR OF STEAM AND WAS SUPPLIED BY ERIE CITY  IN  195
    -------
                                                                                            STATUS  AS UP 0//iO/7
    
    
    
                                                   llM   u  UOM JMJtU)
    
    
    
    
                     HF.hFUPl..«MCt UFbrMPTION K)h l.PtRATlONAL HJI)  SYSThMS ,)M  INDUSTRiAL bORERS
    
    
    
    ii«tA|  rtFiTtftlv. bUoAk!  GtWlMb, l\itBKA.SK»,  I f Ul\i I IMtt i) J
    
    
    
    
    
    
    
    IHt SGKiltiBfcR fFF-LUtNl,  700 GPH FhOH  tAtH SCPUHbFk  iS Stt-iT TO  A  HuMU.
    
    
    
    
    
        IHt  VENTUK1 SCKUBBtHS,, VARIAnLt  uT.MEUR PLUbbr  LtHlbTtK  VbSSfL. AN[)  THE  DtMISTF.H  Akt ALL MADE
    
    
    
    
    UF 3U'. 1.  SS.  Tht IOIAL- 1MSIALLEU CO&T  Of  IHt.  vEMUPI  bCkUbBER  SYSTEM *AS 46<.3fOuO 1 ,M  !975 DOLLARS.
    
    
    
    IHt UPtSAT-ItoK COST F0(-  THE SYSTH-I IS S3«,by(i /YR.
    

    -------
                                                                                     STATUS  AS UF
    
    
    
    
                                        SECTION  <) CCONT1NUEU)
    
    
    
    
                  PERFORMANCE INSCRIPTION FOR OPERATIONAL FGO SYbTtMS  UN  INDUSTRIAL  bUILERS
    INSTALLATION NAME
    
    
    
    
    INSTALLATION LOCATION
    
    
    
    
    SOURCE CHARACTERISTICS
    
    
    
    
    SOURCE RATING
    
    
    
    
    MJwhER OF SEPARATE FGO UNITS
    
    
    
    
    COMTKOL SYSTEM VENOOh
    
    
    
    
    LONTKUL PROCESS
    
    
    
    
    !M£n / RETROFIT
    
    
    
    
    START-UP DATE
    
    
    
    
    CONTROL SYSTEM STATUS
    
    
    
    
    S0
    -------
                                                                                 •        ST«TUS AS UF (ty/jl)/7a
                                            SFCTJON  9 (CONTINUED)
    
                      PERFORMANCE  DESCRIPTION FOK UPtkAUGNAL Ffiu SYSTEMS UN  TNDUblhMAL  UOiLtHS
       INSTALLATION NAME
       INSTALLATION LOCATION
       SOURCE CHARACTERISTICS
       SOURCE RATING
       NUMBER OF SEPARATE FGO UNITS
       CUNTKUL SYSTEM VENDOR
       CONTROL PROCESS
       NEK / RETROFIT
       START-UP DATE
       CONTROL SYSTEM STATUS
       SOd EFFICIENCY
       n/UEK MAKE-UP
       SLUDGE OR BY-PRODUCT DISPOSAL
    
       CONTROL SYSTEM COST
     GREAT  AtbTtKW  SUGAh
     LOvELAMJ,  COLORADO
     COAL  u. dx  SULFUR,  AVERAGE)
     l£l,faOO SCFM  (IOIAL  -  d  BOILERS)
     100,000 ACFM FACh a)  nil)  F
     100,000 LBS/Hf.  STFAM (TOTAL  - d
    GREAT WESTERN  SUGAh
    AMMOMA-LAUEtN  HRuCtSb  WATER
    kFTROFIT
    OCTOBER,  197i
    OPERATIONAL
    30i  (.95  Ld/MM BTll i) TNLETJ
    BOO GPM (PROCESS CUNUEuSATE  hAIFK,  HH=O.7,  L/G=flJ
    wASTtwATtR TREATMENT AND  DISCHARGE  TO RIVER
    EFFLUENT  STREAM  10 HULUING POND
    TOTAL UlbTALLEU COST fijK  THE  TnO  SCkUBBFKS, NEW BREECHING,
    CAPITAL:  sijo.ioo 11974).  THIS  is  TOTAL  INSTALLED COST OF
    THt F60 SYSTEM, l.D. FANS, AND WATER  SYSTEM
    THE FGU SYSTEM.
                                               'OPtR*TlJ»b: »b«,fl-oO/Yh  THIS  INCLUDES ELECTRICITr, STEAM,
                                               MAINTENENCE, LABOR,  ANU  MATERIALS.
    
    
                                            BACKGROUND INFORMATION
         THE  GREAT  WESTERN SUGAR COMPANY HAS Twu cOAL FIRED BOILERS AT  THEIR  LOvELAND,  COLORADO PLANT.
    EACH HolLER  IS RATED  AT  12i,000 LBS/HR OF STEAM; AND BURNS COAL  WITH  0.5d  PERCENT  AVERAGE 5IILFUH,
    •».-* PEKCENT  AVERAGE ASH,  AND AN AVERAGE HEATING VALUE uF 10,i«b  BTU/LB.  TnE  SUGAR FACIORY IS OPER-
    ATIONAL  ONLY 3 MONTHS UF  EVERY  YEAR,  DURING 1 HE FALL OUAKTER.
        THE  FGD  SYSTEM WAS RETROFITTED  TN OCT. '7« AS A PROPRIETARY  DESIGN PRIMARILY FOR  PARTICIPATE
    CONTROL.   THE  FLOE GASES  FROM EACH  BulLER 1100,000 ACFh tf alo F)  PASS  THROUGH  CYCLONES  AND ARE  MIXED
    IN A COMMON  DUCT, AND IH£N  SENT  THROUGH IKU VENTuRJ  bCRUbBERb, WHICH  OPERATE  WITH  A PRESbURt  PROP
    OF 7 I,,. OF  KG AND L/G VALUE  OF  7.i GAL/1000  ACF.  THE  OPERATING GAS  VELOCITY  AT THE  VtMUKl  IM.ET
    IS Hi HPs.   THE SCRUBBERb ARE FOLLOWED  BY  A UEMSTER VES&FL WHICH CONTAINS AN  ONE-PASS,  i-HKEE STAKt
    LHtVERON OEMISTER.  ftASH  WATER  FLUn 1C)  THE PEMlSIfk  IS  ItO GHM, ftlTH  A FkEUUENCY OF Ib  MIN'UTh.b  EVERY
    « HOURS.  THE .PRESSURE DROP  ACROSS  PEMISTEk IS O.S -I |v.  C)F  f,G.   THE EFFLUEM STREAM FkUI. EACH  SCf-'UH-
    UER,  7iO GPM,  IS SENT   TO  A  PuNu, WHICH  (WERFLOwS INTO ANOTHER  HOLDING PONP.
                                                     70
    

    -------
                                                                                       STATUS  AS  OF  07/30/78
    
    
    
    
                                          SECTION  9 (CONTINUED)
    
    
    
    
                    PERFORMANCE OESCKIPTION FOX OPERATIONAL F6D SYSTEMS ON  INDUSTRIAL  BOILERS
    
    
    
    
    GREAT nESTERN SUGAR; LUVELANu, COLORADO (CONTINUED)
    
    
    
    
    
    
        THt VENTURI SCRUBBERSi VARIABLE DIAftTER PLOGS, DEMISTER VESSEL.  AND  THE  ['EMlSTEk  ARE ALL MADE
    
    
    
    
    UF 31h L SS.  THE TOTAL INSTALLED COST OK THE VENTURI SCKUbSER SYSTEM WAS  SliO.SOO IN  197fl DOLLARS.
    
    
    
    
    THE OPERATING COST FOR THE SYSTEM IS $8«,1UO/YR.
    

    -------
                                                                                        STATU?  AS  UF  07/30/78
    
    
    
                                           SECTION  9  (CONTINUED)
    
    
    
    
                     PERFORMANCE DESCRIPTION FOR OPERATIONAL FGD SYSTtMS UN  INPUSTRIAL  BQILfckS
       INSTALLATION NAME
    
    
    
    
       INSTALLATION LOCATION
    
    
    
    
       SOURCE CHARACTERISTICS
    
    
    
    
       SOURCE RATING
       NUMBER  OF  SEPARATE  F6D UNITS
    
    
    
    
       SOURCE  CAPACITY
    
    
    
    
    
    
    
    
       CONTROL SYSTEM VENDOR
    
    
    
    
       CONTROL PROCESS
    
    
    
    
       NEft  / RETROFIT
    
    
    
    
       START-UP DATE
    
    
    
    
       CONTROL SYSTEM STATUS
    
    
    
    
       S02  EFFICIENCY
    
    
    
    
       PArtTICULATE  EFFICIENCY
    
    
    
    
       SLUDGE  OR  BY-PRODUCT DISPOSAL
    
    
    
    
    
    
    
    
       CONTROL SYSTEM COST
     GREAT  WESTERN  SU6AK
    
    
    
    
     SCOTTS  BLUFF,  NEBRASKA
    
    
    
    
     COAL  U.2X  SULFUk, AVERAGE)
    
    
    
    
     65,230  StFM (TOTAL -  2  BUILEKS)
    
    
    
    
     130,000  ACFM tACH al «00  F  (TOTAL  -  ?  BOILERS)
    
    
    
    
     300,(iOO  LBS/HR  STEAM  (TOTAL  -  f  BOILERS)
    
    
    
     a
    
    
    
    
     30 MIN  (TOTAL 2  - BOILERS)
    
    
    
    
     315 MM  BTU/HR  (TOTAL),  31  Mfc (EQUIVALENT);  TUTAL - 2 BOILERS
    
    
    
     GREAT WESTERN  SUGAk
    
    
    
    
     AMMONIA-LADEN  PROCESS WATER
    
    
    
     RETROFIT
    
    
    
    
     OCTOBER, 1975
    
    
    
    
     OPERATIONAL
    
    
    
    
     35% («00 PPM a  INLET)
    
    
    
    
     
    -------
                                                                                        STATUS  AS  OF  U7/M>/7b
    
    
    
    
    
                                           SECTION   9  (CONTINUED)
    
    
    
    
                                DESCRIPTION  FOR  OPERATIONAL KH> SYSTEMS Ofo IM'UST (• IAL  BUlLfcRS
    
    
    
    
    ^Rcftl .,'F-bTtRN SUbAk; SCOTTs ciLUFF,  MtC'KASKA  iCbNTTNUtD)
    
    
    
    
    
    
        IHfc VENTURI SCHDBHtRS, VARIABLE DIAMETER PLUGS,  UEMISTER  VESSEL, AND THE PEMIS1EK  AKt ALL MADE
    
    
    
    
    OF 316 L SS.  THE TOTAL INSTALLED  COST OF  THE  VENTUR1 SCkUBBER SYSTEM ftAS  $7t«,000 IN  197tt DULLAKS.
    
    
    
    
    THE uP£«ATIN6 COST FOR THE SKSTEn  IS $108,100/V«.
    

    -------
                                                                                      .STATUS  AS  UF  07/JO/7B
    
    
    
    
                                          SECTION  9  (CONTINUED)
    
    
    
    
                    PERFORMANCE DESCRIPTION FOR OPERATIONAL FGU SYSUMS ON  INDUSTRIAL BOILERS
      INSTALLATION NAME
    
    
    
    
      INSTALLATION LOCATION
    
    
    
    
      SOURCE CHARACTERISTICS
    
    
    
    
      SOURCE RATING
    
    
    
    
      NUMBER OF SEPARATE FGD UNITS
    
    
    
    
      SOURCE CAPACITY
    
    
    
    
      CONTROL SYSTEM VENDOR
    
    
    
    
      CONTROL PROCESS
    
    
    
    
      NEn / RETROFIT
    
    
    
    
      START-UP DATE
    
    
    
    
      CONTROL SYSTEM STATUS
    
    
    
    
      S02 EFFICIENCY
    
    
    
    
      PARTICIPATE EFFICIENCY
    
    
    
    
      IVATER MAKE-UP
    
    
    
    
      SLUDGE OR BY-PRODUCT DISPOSAL
    
    
    
    
      CONTROL SYSTtM COST
    IT1 RAYOMER, INC.
    
    
    
    
    FERNANDINA BEACH, FLORIDA
    
    
    
    
    BARK AND OIL (£* - 2.5% SULFUR)
    
    
    
    
    201,001) SCFM (TOTAL - £ BOILERS)
    
    
    
    
     a
    
    
    
    
    100 MW TOTAL - « BOILERS; EACH BARK BOILER HAS  A  SCRUBBER
    
    
    
    
    AIRPOL INDUSTRIES
    
    
    
    
    SODIUM HYDHOXIDF SCRUBBING
    
    
    
    
    RETROFIT
    
    
    
    
    1975
    
    
    
    
    OPERATIONAL
    
    
    
    
    80% - 85% (I,?00 PPM A'l INLET)
    
    
    
    
    97X (1.7 GK/SCF AT INLtT)
    
    
    
    
    OPEN LOOP
    
    
    
    
    rtASTEWATER TKEATMENT AND DISCHARGE To TAILINGS  POND
    
    
    
    
    DUCTWORK, AND STACKS.
    
    
    
    
    CAPITAL: $500,000 tmb),  CUST  is FUR s SCRUBBERS,
    
    
    
    
    DUCTWORK, AMD STACKS.
                                           BACKGROUND  INFORMATION
    
    
    
    
        ITT RAYONIER OPERATES AN AMMONIUM-BASED SULFITE PULP  MILL  IN  FERNANDIMA  BFACH,  FLORIDA.
    
    
    
    
    THERE ARE FOUR PROCESS STEAM BOILERS OPERATING  IN  THE FOLLOWING MAiMIMtR:
    
    
    
    
                   NO. 1 - 100,000 LB/HR STEAM- FIRES  FUEL OIL  (NO. 6)
    
    
    
    
                   NO. 3 - 1  USE  IT
    
    
    
    
    FOR THtlK SODA BASE.  LONDdNSATE STEAM Is BF.ING RtCYCLtD  AND USEu FOR  SCRUbRHG  HURPUSES.
    

    -------
                                                                                        STATUS  Ab  UF  D7/jU/7b
    
    
    
    
    
                                                    
    -------
                                                                                        STATUS As OF Oi/SO/Ttt
                                            SECTION  2<> MM  IS FOR  POLLUTION CONTROL
    EQUIt-rtENT, AND S16 MM OF THAI IS  FuR POfctR  PLANT WITH  ITS
    KELATEO POLLUTION CONTROL APPARATUS.
                                            BACKGROUND  INFORMATION
        KEKR-MCGEE CHEMICAL CORP.  HAS  A  NEW  l.J  MM  TuN/r*  SOOA  ASH PLANT AT 1RONA,  CALIFORNIA.  THE
    PLANT, LOCATED ALONG THE SHORE  OF  SEARLES  LAKE,  IS  TnE LARGEST Y£T  BUILT TO YIELD SUUA ASH BY DIRECT
    CAhrtONATION OF BRINE AND ^AS CUMMIbSlONEo  IN  JUNE   1978.   THt PROCESSING HVNUVATIONS,  tvHICH
    HAVE IMPROVED THE PLAM EFFICIENCY,  INCLUDE  CAR80NATION  UNDER 13.5  L8/56.  IN.  PRtSSUKE, USE OF
    A COAL-FIRED PO«tR PLANT, AND  RECOVERY OF  CO* MOM  THE  FLUE  GASES.
       THE PLANT HAS uo BOILERS,  EACH RATED AT  ^ Mft.  «HTCH  PROUOCE  PROCESS SIEAM  AND  ELECTRICITY.
    EACH BOILER PROOOCES 6^0,OuO LdS/HK  OF STEAM  AT  1SOO PSI  AND  8oRNS  A *[XTUKE  OF WESTERN COAL
    (0. ! PERCENT SULFUR) A.^0 PETROLEUM COKt  (l.b  PfeRthNT SULFUR).   THE  HItH SULFOf-  CoKE IS MIXED IMTH
    IHL CI.AL I:. OROER TO I«PKOVE TnE PART1CAL  IGNUAtluN A,vO  IN  TORN  FLY-ASH COLLECTION IN THE ESP
    .'.MiCri OPERATES ON THE uOLD SIDE OF THE P*FHEATER AT 98.5  PtRCENT  EFFICIENCY AMJ iOO F.  THE FLUE
    bAS HLO. RATt FRUM EACH BOILER  IS 363,u«u  ACFM A) 3^0  f AM, MAY CONTAIN SOc' bMNLEN i3b TO 5985 PPh
                                                    7fc
    

    -------
                                                                                      STATUS  AS  UF  07/30/76
    
    
    
    
    
                                          SECTION  9 (CONTINUED)
    
    
    
    
                    PERFORMANCE DESCRIPTION FOk OPERATIONAL FGu SYSTEMS ON  INDUSTRIAL BOILERS
    
    
    
    
    KFRR-MUGtE CHEMICAL COKP.; TrtONA, CALIFORNIA (CONTINUED)
    
    
    
    
    
    
    UEHEMHNG UPON THE FUEL.  THE AIM POLLUTION REGULATIONS DICTATE  THAT  EACH  BOILER  MAY  RELEASE NOT
    
    
    
    
    wtjKh TnAi\ 10 LbS/HR PARTICULATE, 200 LBS/HK OF SU2  AND  IflO  LbS/HR  OF  NOX.
    
    
    
    
        IHt FLUE GASES ARE SCRUBBED bY  THE END LIQUOR FRuM  THE  SODA  ASH PLANT  IN TWO  SCRUBBERS
    
    
    
    
    130 FT DIA X Ji FT HICH EACH] WHICH ARE MILD STEEL  VESSELS  KITH  FLAKE LINING AND  POLYPROPYLENE  SIEVE
    
    
    
    
    TKAY8.  THE TOP TRAY RECEIVES PLAIN WATEK  WHEREAS THE SECOND  T*AY  RECEIVES THE  RECIRCULATING LIQUOR
    
    
    
    
    AT CM OF 6 - 6.5.  THE SPENT L13UOR FROM  THE BOTTOM OF  THE  SCRUBBERS  IS HEC IwCULATED  BY RUBBER
    
    
    
    
    LINED PUMPS TO A MILD STEEL SURGE TANK WHERE FRESH  END-LIQUOR IS ADDED TO  IT WITHOUT  AGITATION.  A
    
    
    
    
    BLEED OFF STREAM IS CONTINUOUSLY TAKEN BACK  TO THE  SALT PONDS.
    
    
    
    
        THE BOILER 1.0. FANS  (1600  HP.) FORCE  THE GASES THROUGH THE  SCRUBBERS  AND EXPERIENCE  6 IN.  WG
    
    
    
    
    PRESSURE DROP.  THE FANS  HAVE MILD  STEEL  CASING.  1 HE DOWNSTREAM DUCTWORK  IS MILD STEEL WITH FLAKE
    
    
    
    
    LINING WHEREAS THE STACK  IS CONCRETE WITH  FRP LINER.  AMdIENT AIR IS  HEATED IN AN EXTERNAL
    
    
    
    
    STEAM HEATER AND MIXED WITH  THE EXIT FLUE  GASES  TO  INCREASE THE  TEMPERATURE FROM 125 F Tu ABOUT
    
    
    
    
    175 F.  AT MAXIMUM LOADING,  THE SCRUBBERS  HAVE  A  SU8 REMOVAL  EFFICIENCY OF 9B PERCENT.   THE SCRUBBED
    
    
    
    
    FLUE  RASES WILL 13E PROCESSED  THRUUUH  TWO  MONOET HANOLAMINE (MEA)  PLANTS FUR EXTRACTION OF C02.  EACH
    
    
    
    
    PLANT WILL PRODUCE 300  TONS/DAY OF  C02  AND WILL  BE  THE  MAIN SOURCE OF MAKEUP C02 IN THE  CARBONATION
    
    
    
    
    
    PLANT.
    
    
    
                                              OPERATING  HISTORY
    
    
    
    
    1ST QIIARTER-1978    THE MAJOR CONSTRUCTION WORK  (VAS OVER. PRECOMMISSIONING ACTIVITIES V»ERE UNDERWAY.
    
    
    
    
    THE PLANT  WAS PROJECTED  TO  GO  OlMSTRtAM  tiY APRIL  1. 1978.
    
    
    
    
    
    
    
    
    
    2ND UlllARTER-1978    THE FGD  SYSTEM  WAS  COMMISSIONED DURING THE REPORT PERIOD. THE BOILERS WERE  RUN
    
    
    
    
    TO  FULL CAPACITY WITH  100 X  OIL FEED.   COAL AND  COKE WERE USED UP TO 80 X OF THE FUEL.   1 HE MAJOR
    
    
    
    
    STARTUP PROBLEM WAS  FRAY  TIEOOrtN.   THE  POLYPROPYLENE SIEVE TRAYS WERE NOT STRONG ENOUGH  TO TAKE  THE
    
    
    
    
    LOAD  OF  INVENTORY  LlUUIO. THESE WILL  BE  REPLACED  BY 31faL  SS OR A HIGHER GRADE ALLOY.  ThE PRESENCE  OF
    
    
    
    
    CHKOK.ATE  IONS  IN  THE  MAKtUP  WATER  CAUSED SOME  CONCERN.
                                                     77
    

    -------
                                                                                        •STATUS AS OF 07/30/76
                                           SECTION  9  (CONTINUED)
                     PERFORMANCE DESCRIPTION FOR OPERATIONAL FGu SYSTEMS  ON  INDUSTRIAL  BOILERS
       INSTALLATION NAME
       INSTALLATION LOCATION
       SOURCE CHARACTERISTICS
       SOURCE RATING
       NUMBER OF SEPARATE FGO UNITS
       SOURCE CAPACITY
       CONTROL SYSTEM VENOOR
       CONTROL PROCESS
       NEW  /  RETROFIT
       START-UP DATE
       CONTROL SYSTEM STATUS
       S0£  EFFICIENCY
       PARTICIPATE  EFFICIENCY
       SLUDGE  OR BY-PRODUCT  DISPOSAL
      CONTROL SYSTEM COST
     MEAD  PAPERBOARO CO.
     STEVENSON,  ALABAMA
     OIL  (1.5*  -  3X  SULFUR)
     100,000  ACFM 3  450 F  (TOTAL - 2 BOILERS)
      1
     SO M(V  (EQUIVALENT);  TOTAL  - TfcO BOUtRS
     AlkPOL INDUSTRIES
     SODIUM HTDKOXIDE SCRUBBING
     NEW
     1975
     OPERATIONAL
     95* (1,500 PPM  S INLET)
     90%
     ALKALINE SULFITE/BISULFITF.  RECYCLED  TO  PULP  PROCESS
     RECOVERED SOLUTION USEj AS  MAKE-uP TO COOKlNb  LIuUOR  IN PULP
     MILL.
     CAPITAL:  $173,000 (197*1).   THIS  *AS  THE ORIGINAL
     EQUIPMENT ANU INSTALLATION  COSI.  SINCfc IHfcN EXTENSIVE
    MODIFICATIONS HAVE BtEiv REQUIRED.  ANOTHER 173,000  WAS  SPENT
    FOR REPAIRS  ANU UPGRADING  IN  1976.   UVER  THE SCRUBBER PLANT
    LIFE,  AN  ADDITIONAL 136,000 HAS  BEEN SPENT,  INCLUDING:
    35,000 (RUBBER LINERS), 51,000  (STAINLESS STEEL LINERS),
    AND 47,000 (GENERAL REPAIRS).
                                              OPERATING:  s
    -------
                                                                                       STATUS) *S OF G7/31I/7B
    
    
    
    
    
                                          SFCTIOlv   9  ICONTlMjFti)
    
    
    
    
                    PERFORMANCE DESCRIPTION F OK  OPERATIONAL  H-u  SYSTtMS UN TivDUfrT >• 1 AL BOILERS
    
    
    
    
    MEAD PAPtRSOARO CO.; STEVENSON, ALAHAMA (COM li'vUtl'J
    
    
    
    
    
    
    THE ABSORBER SECTION AND PASSES UP -THROUGH  THREE  V UBBLt-C AH  TR* Yb.   A SClilU^ CARbONAlE SOLUTION  IS
    
    
    
    
    INTRODUCED THROUGH A BANK OF 1.5  INCH NOZZLES  W> SPIM VANtS.   IhF  GAS FXI1S THROUGH A FIBERGLASS"
    
    
    
    
    STACK.  SCRU3BER EFFLUtN] 1600 6PMJ , MuSTLY  SOuIuM  SuLFITE,  IS ScNT 10 ThF MILLS PULPING OPERATION'S
    
    
    
    
    FOR EVENTUAL USE IN  1HE DIGESTERS.   PH  IS CONTROLLED Al  7.U-b.i> IN  THF. REC IRtMLAT ION 1AMK.
    
    
    
    
         THE S02 SCKUBtJlNG SYSTEM  WAS  DOftN  FKOM  MAnCrt IHKOUGH  JULY 197fe DUE  10 AtikASJO^ PROBLEMS.  TnE
    
    
    
    
    A8KASION WAS CAUSED  PARTIALLY  &Y  HIGH STKEAM VELOCITY IHKOU&M THE tXISIEM VEMOKl PARIltULAH
    
    
    
    
    SCRUBBER I«TO  THE S02 SCKOUBER.   SODIOfi LAr-BONATE AM) CAKROfc PAKTICLES THAT  HAD  NOT KONt IMl)  SOLU-
    
    
    
    
    TION ALSO WERE VERY  ABRASIVE TO THE. SO? SCRUBBER  HN1MU.  IN AOniTION. THE ORIGINAL bLASS-FlAKEO
    
    
    
    
    LINER  (5 MM THICK) WAS EXPERIENCING STRESS  ChACKlf.b.
    
    
    
    
         THE HIGH  VELOCITIES  IMTWOUUCEu BY  THE  VENlUkI  hERh  ELIMINATED BY kFMOVING THE PAR11C.ULA1E
    
    
    
    
    VENTURI SECTION OF  THE SYSIEM.  THE KLASS-FLAKtD  LINING WAS HAIChED wIlH  SbO.DUO WURTH  OF
    
    
    
    
    CAKPtNTEH 20 LINER.   THESE  CORRECTIVE  ACTIONS HELPED FOR A WHILE, 8UT AS  II  1URNtP OUT,  THE CARPEN-
    
    
    
    
    TER <>0 rtAS NOT INSTALLED  PROPERLY  AMU  SOLU1IUN WAS GETTING BETWEEN IT AND  THE  MILD STEtL SHELL.   IT
    
    
    
    
    WAS FINALLY DECIDED  TO  INSTALL NEW RUBBER  LINING  INSIDE THE ENTIRE SCRUBBER,  INCLUDING  THE  SPIN
    
    
    
    
    VANES, AT A COST OF  *15>0,000.   TO PREVENT  ANY HEAT PROBLEMS, ADDITIONAL  NU2ZLFS  WERE  1NS1ALLEO.   TO
    
    
    
    
    UATE,  NO MAJOR PROBLEMS  HAVE OCCURRED  KITH  THE RUBBER LINING.
    
    
    
    
    
    
    
    
    
                                              OPERA!ING HISTORY
    
    
    
    
    
    -------
                                                                                        STATUS  AS  OF  07/30/78
                                           SECTION  9  (CONTINUED)
                     PERFORMANCE DESCRIPTION F()K OPERATIONAL FGu SYSTEMS ON  INDUSTRIAL  BOILERS
       INSTALLATION NAME
       INSTALLATION LOCATION
       SOURCE  CHARACTERISTICS
       SOURCE  RATING
       NUMBER  OF  SEPARATE  F60 UNITS
       SOURCE  CAPAClTr
    
       CONTROL  SYSTEM VENDOR
       CONTROL  PROCESS
       NErt  / RETROFIT
       START-UP DATE
       CONTROL  SYSTEM STATUS
       SOd  EFFICIENCY
       HATER MAKE-UP
       SLUO&F OR  bY-PROOUCT  DISPOSAL
    
       CONTROL SYSTEM COST
    MINN-DAK  FARMER'S  COOPERATIVE
    ftAHPETUN, NORTH  DAKOTA
    LIGNITE  11.OX  SULFUR)
    160,000  ACHM 5) 3bO F  (TOTAL  -  d  BOILERS)
     ?
    ba Mh  (EQUIVALENT); TOTAL  -  2  BOILERS
    1WO BOILERS, EACH  id 275,000  LBS/HR  STEAM  (£50 PSIG - 155 F)
    KOCH ENGINEERING
    AMMONIA SCRUBBING
    RETROFIT
    JUNE,  1977
    OPERATIONAL
    TESTS  INCONCLUSIVE.
    200 GPM POND WATER
    WASTEWATER TREATMENT                     .     .
    BLEED STREAM GOES TO AN ACTIVATED SLUDGE SYSTEM  a)  160  GPM
    CAPITAL: $300,oou  (1977).  TOTAL EQUIPMENT COST.
                                            BACKGROUND  INFORMATION
        MINN-OAK FARMER'S COOP. HAS  A  SUGAR  FACTORY  AT  WAHPElOu,  NORTH OAKOTA.  THERE ARE TWO BOILERS,
    EACH WITH A CAPACITY OF £75,000  LBS  STEAM/HR  AT  dSu PSIG  AND  «bS F.   THE FUEL BURNED IS 1% SULFUR
    LIGNITE.  SULFUR DIOXIDE REMOVAL IS  EFFECTED  BY  AMMONIA  ADDITION TO  THt RECIRCULA T ING SCRUBBER
    LIQUOR.
        KOCH ENGINEERING HAS SUPPLIED  TWO SCRUBBERS  FOR THE  BOILERS  EACH OF WHICH GENERATES 135,000 ACFM
    OF FLUt GASES AT 350 F.  T ME SCRUBBER SYSTEMS  ftE.MT  ONSTREAM  IN JOIME  77.  EACH SCRUBBER IS A VARIA8LE
    THROAT VENTURI WITH OPLN ENDED PIPE  INLETS FOR LIHUID  ANo  WAS PR1MARLY  DESIGrtEU FOR PARTICULATE
    CONTROL.  THE SCRUBBER LK4UOR IS RECIRCULA1ED  AT A  RATE  OF 800 GPM AND  THE BLEED-OFF RATE GOING TO
    THt ACTIVATED SLUDGE SYSTEM IS IbO GPM.  THE MAKEUP PO.MO  WATER FLOW  KAIE IB dOO (,P«.  THc PRESSURE
    DROP ACROSS A SCRUBBER IS 11 IN. WG.  IHERE IS Oh.E  CUMMON  CHEVERuN TYPE UEMISltR AND ONE  STACK.
    I HE INLF.1  CONCEN1RATION KANGES ARE 76-193 LBS/HR OP  M^  ANu  .3-.4  GR/SCF OF PARTICULATE.   THE OUT-
    LET CONCENTRATION RANGES ARE 10-37 LWS/HK AND  .027-.030 GR/SCF RESPECTIVELY.
        THE SCRUBBERS ANu I HE LluUuR INLET PIPtS ARE MAUL  uF  ;
    -------
                                                                                        STATUS  AS  OF  07/30/78
    
    
    
    
                                           SECTION  9  (COM 1NUFD1
    
    
    
    
                    PEKFURMANCt  UESCKIPTION H>k UPtRATlOuAL  F'Gu  bYSTtMS ON INDUSt^IAL BlJILtKS
    
    
    
    
    MT^N-DAK FARMER'S COUF't«ATlVt ;  (VAHPtTur
    -------
                                                                                    •STATUS AS OF 07/30/78
    
    
    
    
                                         SECTION  9  (CONTINUED)
    
    
    
    
                  PERFORMANCE DESCRIPTION FOR OPERATIONAL  FGu  SYSTEMS  UN  INDUSTRIAL BOlLfcRS
    INSTALLATION NAMt
    
    
    
    
    INSTALLATION LOCATION
    
    
    
    
    SOURCE CHARACTERISTICS
    
    
    
    
    SOURCE RATING
    NUMBER OF SEPARATE FGD UNITS
    
    
    
    
    SOURCE CAPACITY
    
    
    
    
    CONTROL SYSTEM VENDOR
    
    
    
    
    CONTROL PROCESS
    
    
    
    
    NEW / RETROFIT
    
    
    
    
    START-UP DATE
    
    
    
    
    CONTROL SYSTEM STATUS
    
    
    
    
    SOa EFFICIENCY
    
    
    
    
    SLUDGE OR BY-PRODUCT DISPOSAL
    
    
    
    
    CONTROL SYSTEM COST
    MOBIL OIL COMPANY
    
    
    
    
    SAni ARDO, CALIFORNIA
    
    
    
    
    OIL (2. (1% - 2.d« SULFUR)
    
    
    
    
    182,000 SCFM  (TOTAL - 30 BOILERS)
    
    
    
    
    8000 ACFM a 470F, FOR tACH  OF  d'd FGD  SYSTEMS
    
    
    
    
    18,000 ACFM oi <470F, FOR tACH OF b  FGD SYSTEMS
    
    
    
    30
    
    
    
    
    60 Mn CEUUIVALtNI); btO MM  BTU/HR:  TUTAL  -  3U  BOILERS
    
    
    
    
    MOBIL OIL COMPANY
    
    
    
    
    SOUIUM HYDROXIDE SCRUBBING
    
    
    
    
    RE1RUF1I
    
    
    
    
    1971
    
    
    
    
    OPERATIONAL
    
    
    
    
    tOU tlbOo PPM 
    -------
                                                                                       STATUS  Ay  UF  07/il'/7u
    
    
    
    
                                          btLTION  9 (LONT If>uEu)
    
    
    
    
                    PERFGRMANCt DESCRIPTION MlK OPfcRATlOKAL hfcii SYSUMS UN  1 NDuh 11-i AL  BOILERS
      INSTALLATION NAME
    
    
    
    
      INSTALLATION LOCATION
    
    
    
    
      SOURCE CHARACTERISTICS
    
    
    
    
      SOURCE RATING
    
    
    
    
      NUMMER OF SEPARATE FGO UNI IS
    
    
    
    
      SOURCE CAPACITY
    
    
    
    
      CONTKOL SYSTEM VENDOR
    
    
    
    
      CONTROL PROCESS
    
    
    
    
      NEW /  RETROFIT
    
    
    
    
      STARI-UP DATE
    
    
    
    
      CONTROL SYSTEM STATUS
    
    
    
    
      S02 EFFICIENCY
    
    
    
    
      PARTICuLATE EFFICIENCY
    
    
    
    
      WATER  MAKE-UP
    
    
    
    
      SLOOGE OR BY-PRODUCT DISPOSAL
      CONTROL SYSTEM COST
    NEKOUSA PAPERS, INC.
    
    
    
    
    AShDGWN, AhKANSAb
    
    
    
    
    LOAL (1X-1.VA SULFlik)
    
    
    
    
    ell,UUO sCfl" Si 3bb F (TOTAL -  1 BOHERJ
    
    
    
    
     I
    
    
    
    
    10U H.W  (LfOUlVALFNT) ! DESIGN -  bOu,0(!0  LB/HK  bTEAH
    
    
    
    
    AlkPCL  INni'SIMFS
    
    
    
    
    LAuSTIC bCKUBBiNU
    FEbRUARY,
    
    
    
    
    OPERATIONAL
    
    
    
    
    90 + X (600 HPM ill INLET)
    
    
    
    
    9B% - 99* 11.42 GR/SCF Al  INLET)
    
    
    
    
    OPEN LIUip
    
    
    
    
    AL^ALINE SULKITE/B1SULFITE  RECYCLED  TO  PULP PROCESS
    
    
    
    
    S0£ RECOVERED FROM SODIUM  StILF I TE/SHLFATE  LIUUOR AND RE-
    
    
    
    
    CYCLED TO PULP1NU PROCESS.
    
    
    
    
    CAPITAL: Sc?50,ooo 11973).   THIS  is  THE  EQUIPMENT COST.
                                           BACKGROONi)  INFORMATION
    
    
    
    
        THE NEKOOSA-EDWARDS PAPER PULP MILL IN AShDOrtN,  AfiRANSAS HAS  TWO  AIRPOL SCRUBBERS ON A 50-Mrt
    
    
    
    
    EQUIVALENT STEAM 801LEK FIRED WITH COAL OR FUEL OIL.   THE  VENlURI  SCRUBBERS ARE UESIIiNED TO REMOVE
    
    
    
    
    BOTH SULFUR DIOXIDE AND PART ICULATES.  THE IMENI  OF  NEKOOSA-EDnARDS  ftAS TO MAKE, FROM THE SCRUBbFK
    
    
    
    
    EFFLUENT, SALTCAKE WHICH WOULD BE USED AT THE MILL.  I HE  COAL HAS  1-1.5* SULFUR AND A HEATING VALUE
    
    
    
    
    OF 12,000 BTU/LB. IT IS BURNED AT A RATE OF  27 TONS/HR.
    
    
    
    
        THE SCRUBBER HANDLES 325,000 ACF« AT 355 DEGREES  F.   SCRUBBER  INLET S02 CONCENTRATION
    
    
    
    
    IS TYPICALLY 600 PPM WITH A PART1CULATE LOADINb UF 1.U2  &K/SCFM.   RECIRCULATtD WATER IS dLED
    
    
    
    
    OFF AT lbO-250 GPM.  REAGENT MAKE-UP AMOUNTS Tu 1 ? LC/hlN  OF SODIUM HYDROXIDE.  SCRUBBER UlMUERFLUW
    
    
    
    
    CONSISTS OF FLYASH AND A SOLUTION OF SODIUM  SULFllE/SULFATt.   THE  ASh SLUkRY G'UES TO A SETTLING
    
    
    
    
    POND.
    
    
    
        THE PREDOMINANT DIFFICULTIES WITH THE FGD SYSTEM HAVE  BEEN IwO-FOlD.  FIRST, THE PLANT HAS BEEN
    
    
    
    
    UNABLE TO DEVELOP AN ADEQUATE PH CONIROL MECHANISM.   THE PH CONTROL SYSTEM MONITORS THE AMOUNT Uh
    
    
    
    
    CAUSTIC AGENT, I.E., SODIUM HYOROXlOfc, WHICH GOES INTO THE RECYCLE TANK, KEEPING THE PH OF THE
    
    
    
    
    SCRUBBER SOLUTION AT A NONCO«ROSIVE LEVEL,   THE PLANT  HAS  BEEN PLAGUED KITH PROBLEMS ii\
    
    
    
    
    OPERATING THE PH CONTROL SYSTEM AND HAS SUFFERED  A GREAT DEAL  OF  CORROSION.  THE SECONO PROBLEM
    
    
    
    
    CONCERNS THE CHEMICAL REGENERATION PORTION OF 1 HE  SYSTEM.   THE INTENT OF THF PLANT WAS TO SEPARATE
    
    
    
    
    THE FLY ASH FROM THE SCRUBBER LIQUID AND TARE THE SCRUbBER LIQUlu  THROUGH A SERIES OK EVAPORATORS
    

    -------
                                                                                       STATUS AS UF 07/30/78
    
    
    
                                           SECTION  9 (CONTINUED)
    
    
    
    
                     PERFORMANCE DESCRIPTION FOh OPERATIONAL FGO SYSTEMS ON INDUSTRIAL BORERS
    
    
    
     «EM.)USA PAPERS,  INC.;  ASHDOWN,  AKKAMSAS (CONTINUED)
    
    
    
    
    
    
    
     -HtRE SOUIUM SULFAIE,  I.t., SALTCAKE.  WOULD BE GENERATED.  THE PLANT HAS BEEN UNABLE TO OPERATE THE
    
    
    
    
     FLY  ASH SEPARATION SYSTEH PROPERLY,  AND THERE IS NOT ENOUPH EVAPORATION CAPACITY FOR THE PLANT TO
    
    
    
    
     PROCESS THE  SCRUBBER  EFFLUENT  AT  FULL  OPERATIONAL CAPACITY.
    
    
    
    
    
         IN  SPITE OF  THE OPtRATIONAL PROBLEMS,   THE SoLFUK DIOXIDE  AND PARTICULATE REMOVAL EFFICIENCIES
    
    
    
    
     UF  THE  FSD  SYSTEM  ARE  90  AND 99 PERCENT,  RESPECTIVELY,  ACCORDING TO 1 HE PLANT ENGINEER.  THE WASTE
    
    
    
    
     PRODUCT FROM THE SCRUBBER IS NOT  RECYCLED,  AT  PRESENT,  AND  IS  PUMPED 10 IHE HASTENATER TREATMENT
    
    
    
    
     PLANT.   CLEANED  WASTEwATER  IS  RETURNED Tu  THE RIVEK.
    
    
    
    
    
         UPON STARTUP,  PROBLEMS  OCCURED MTH THE  PIPING  AND  VALVES  MICH WERE CONSTRUCTED OF CARBON
    
    
    
    
     STEEL.   THE  CARBON STEEL  SYSTEM WAS  REMOVED  AND  REPLACED  WITH  STAINLESS STEEL VALVES AND PIPING.
    
    
    
    
     SfME  PIPING  LEAKS  OCCURRED  AND WERE  REwELDED.   SuME CORROSION  OF DUCT  DAMPERS OCCURED AND WERE RE-
    
    
    
    
     LIEVED  8Y ADJUSTING THE PH  OF  THE SCRUBBING  LIQUOR.  THE  PH IS MAINTAINED  BETWEEN b.5 - 6.0.
    
    
    
    
         THE SCRUBBER SYSTEM OPERATES  WITHOUT REHtAT,  EXHAUSTING TO A FIBERGLASS COATED STACK.  PARTIC-
    
    
    
    
     ULARS  ARE CONTROLLED  WITH  CYCLONES  AND  TWO  VARIABLE THROAT VENTURI SCRUBBERS WITH AN AVERAGE  PRES-
    
    
    
     SUKE  DROP OF  14 TO Ib  INCHES W.G.
    
    
    
    
    
                                             OPERATING  HISTORY
    
    
    
    
     3RD QUARTER-1977    NO MAJOR PROBLEMS  HAVE BEEN  REPORTED.
    
    
    
    
     CO,
    -------
                                                                                     STATUS  AS  uF 07/30/7B
                                         SECTION  9 (CONTINUED)
                   PERFORMANCE OESCKIPT ION FOR OPERATIONAL FGO SYSTEMS UN  INDUSTRIAL BOILERS
     INSTALLATION NAME
     INSTALLATION LOCATION
     SOURCE CHARACTERISTICS
     SOURCE RATING
     NUMPtfl OF SEPARATE FGD UNITS
     SOURCE CAPACITY
     CONTROL SYSTEM VENDOR
     COfcTrtOL PROCESS
     NEW / RETROFIT
     START-UP DATE
     CONTROL SYSTEM STATUS
     SClc. EFFICIENCY
     (-ARTICULATE EFFICIENCY
     WATER MAKE-UP
     SLUDGE OR BY-PRODUCT  DISPOSAL
    
     CONTROL SYSTEM COST
    RICKtNBACKER AIR FORCE BASE
    COLUMBUS, OHIO
    COAL (i.bX SULFUR)
    30,000 SCFM (1 BOILER)
     1
    20 Mft (EQUIVALENT)
    RESEARCH-COTTRtLL/BAHCU
    LIMESTONE SCRUBBING
    RETROFIT
    MARCH, 1976
    OPERATIONAL
    90* (AVERAGE)
    98%
    OPEN LOOP - 2.b  6PM/hl»  (MAX)
    NON-FIXATED SLURRY  TU LINED  POND
    UNSTABIL1ZED  CAS03/S04  SLUDGE  TO  LINED PONU
    CAPITAL:  $
    -------
                                                                                       'STATUS AS OF 07/J50/7B
                                           SECTION  9  (CONTINUED)
                     PERFORMANCE DESCRIPTION FOR OPERATIONAL  FGu  SYSTEMS  0*  INDUSTRIAL  BORERS
     RICKENBACKER AIR FORCE BASE? COLUMBUS, OHIO (CONTINUED)
    
     SCRUBBER TOWER, LIMESTONE STORAGE AND HANDLING SYSTEM, CLARIFItR,  BOOSTEK  FAN  AND  ASSOCIATED  DUCT-
     WORK, PUMPS, CONTROLS, AND A SLODGE DISPOSAL POND.
         SOLID PARTICULATE AND SULFUR DIOXIDE-LADEN FLUE GAS  TAKEN FRUM EACH UF  THF EXISTING  SFVf.N
     STACKS IS FED THROUGH A COMMON HEADER AND INTO A MECHANICAL COLLECTOR .HERE PRIMARY PAKTICULATE
     REMOVAL TAKES PLACE.  1 HE MECHANICAL COLLECTOR HAS A DESK,,, REMOVAL EFFICIENCY OF  ,0 PERCENT  AND
     WAS INSTALLED PRIMARY TO RtDUCE FAN .EAR.  THE .PARTLY CLtANEu GAS THEN FLO.S JNTO THE  BACHO  ,0WER
     WHERE ADDITIONAL PARTICULATE AND PRIMARY  SULFUR DIOXIDE REMOVAL TAKES PLACE.
         THE BACHO SCRUBBING VESSEL IS A  VERTICAL TOWER CONSISTING UF T*0 SCRUBBING STAGES. GAS  FLOWS
     THROUGH THE  TOWER  «H£RE IT IS  CONTACTED  WITH A LIMESTONE SLURRY.  AFTER PASSING THROUGH  THE
     FIRST  SCRUBBING STAGE,  ENTRAINED MOISTURE  IS REMOVED BY A CYCLONIC TYPE MIST FLIMINATOR.  THE
     GAS THEN  PASSES THROUGH A  SECOND SCRUBBING  STAGE  AND A  SECOND CYCLONIC MIST ELIMINATOR.   THE
     CLEANEU GAS  IS  DISCHARGED  TO  THE ATMOSPHERE THROUGH A  STUB STACK ATOP THE  ABoORBER  ToWLR.
         FINE  MESH LIMESTONE  IS EMPLOYED  AS  THE  REAGENT  IN  THE SCRUBBING SYSTEM.  THE  SCRUBBING SLURRY IS
     THEN PUMPED  TO  THE  ABSURBER  WHERE IT  IS CONTACTED  W!TH  THE FLUE  GAS IN A CUUNTERCURRENT FASHION.
         THE SPENT SCRUBBING SOLUTION IS  DISCHARGED  TO  THE  THICKENER  WHERE THE  WASTE SOLIDS  SETTLE OUT.
     THICKENER OVERFLOW  IS RETURNED  TO THE NIx/HOLO  TANK.   THICKENER  UNDERFLOW  IS DISCHARGED TO A 5-
     ACRE HYPALON-LINED  DISPOSAL POND.  THIS POND IS LOCATED APPROXIMATELY  «0o  FEET  FROM ,HE ABSORBER
     TO.ER.  CLEAR WATER  FROM THE POND  IS RETURNED  TO THE PROCESS  AS  MAKE-UP  MTEK  JN  THE  SLUKRY  1ANK.
    
    
                                             OPERATING  H1SIORY
         THE SYSTEM WAS  INITIALLY PLACED  IN SERVICE MARCH U,  ,976.   INITIAL  OPERATION PROCEEDED  IN AN
     OPEN WATER LOOP MODE BECAUSE THE  THICKENER WAS NOT  YET  COMPLETELY  INSTALLED.  SULFUR DIOXIDE IN-
     LET CONCENTRATIONS WERE IN THE  1800  TO 2000 PPM RANGt.  HIGH OXYGEN CONCENTRAT!ONS  ALSO EXIST  IN
     THE FLUE GAS BECAUSE THESE OLDER. INEFFICIENT BOILERS OPERATE AT IbO TO  160  PERCENT EXCESS AIR
    RATES.  SULFUR DIOXIDE REMOVAL EFFKIENCY  HAS BEEN  !N THE LOW 90 PERCENT PLUS RANGE.  EARLY
    PROBLEMS WERE PRIMARILY UF A MECHANICAL NAIURE USUALLY  ASSOCIA.ED WITH START-UP.  THE MAJOR  START-
    UP PROBLEMS  WERE AS FOLLOWS:
             1.  ELECTRICAL CIRCUITS AND SYSTEM CONTROL  PANEL.
             2.  PUMP MALFUNCTION-SPARE PARTS  SHIPMENT  DELAY.
             3.  SEDIMENTATION  BUILDUP IN  THE  SCRUBBER VESSEL (THIS WAS (HIE PRIMARILY TO OPERATION  AT
                HIGHER  THAN DESIGN  SOLIDS CONCENTRATION IN  THE SCRUBBING SOLUTION BECAUSE IHt  THICKENER
                WAS  NOT  YE1  IN  SERVICE PLUS  GRIT GETTING THROUGH THE LIME SLAKER RKII  REMOVAL  STEP).
            «.  FAMILIARIZATION OF  THE OPERATING STAFF  WITh IHE MECHANICS OF THE PROCESS.
            5.  I.D.  BOOSTER FAN PROBLEMS.   ADDITIONAL  BRACING, AND  EPOXY GROUT I Ml WAS REQUIRED TO STOP
            THE  ELEVATED FAN CONCRETE SUPPORT FROM VIBRATlNb WHILE  IHE FAN AAS OPERATING.
                                                    Bfe
    

    -------
                                                                                        .STATUS AS UF" U7/30/7M
    
    
    
    
    
                                           SECTJt'1-J  "9 ICOf-Jl 1 MJFU)
    
    
    
    
                                 OESC>< TFT 10i\  FOR OPt .RA I 1 Ut.»L FGu SYSTEMS  UN  INDUSTRIAL BOH.tKb
    
    
    
    
    
    RICKfcNbACKER AIR FuRCt SASt!  CuLJMbUS,  Onlu (Ci,i\ I 1 Mil tfi J
    
    
    
    
    
    
    ,MOv/. 76 IHROUGH JUN.  77     DUWNTIf'f  ft*S  LESS THAT, 6%.  OPERATING  PRObLtKS HAVb BEEN rFCHANlCAL AUO
    
    
    
    
    CONTROL RATHER THAM PROCE SS-HEL A IE U.   FAN-RELATED PRuBLEMS  ACCOUNTED FUR I VtR 75* uF THE ACTUAL
    
    
    
    
    DOWN-TIME.  THIS RESULTED  FROM  EXCESSIVE FAN VJ8RATTUNS CAUSED  BY  BEARING,  SUPPORT, AND  INSTRUMENT-
    
    
    
    
    ATION UIFFICULTIES.   IN  APRIL 19/7.  I Ht  FAiv viHlF.L DEVELOPED A  (.RnCx,  IN  Tut  Rir AITKIBI1TLO  T (I
    
    
    
    
    FAlTbllc FROM RESUNAMT  VIBRATION.   THE  FAN ftAa S,E,,T B«Cn TO  THE'  MANUF ATI IJKFK,  AMERICAN STANDARD,  wHU
    
    
    
    
    MADE THE REOUIKED.MODIFICATIONS.   Tht  UPIGINAL FAN AAS RADIAL  oLADE  WTIh KIMb, A,JD  A MAJUR  MuniFI-
    
    
    
    
    CATION WAS CHOPPING THE  .VIMS OFF,  ThcRtwv KELiiciivt THE HIAMEIEU.   int FAH WAS KFTUKNEU  IN  EARLY  MAY
    
    
    
    
    AMI) IHE VIBRATION  PROBLEM  WAS SOLVED.   OTHER OF'EKAT I ufci, ir.ERF  RtLATlVLLY PRuPLF M-F REE.   THfcKE  WERE
    
    
    
    
    NO CORROSION, EROSIOK,  SCALINK,  OR PLUbGlNfe PROBLEMS.  THE  SYSTEM bF.GAN RIIIMNlNt;  UN  LIMESTONE  IN
    
    
    
    
    APRIL, A3 PART OF  THE fcPA  TEST  PKd&KAM.  LIMESTONE PtRFOtjD NO.  3 WILL BE ON bTANuiJY.   IIE-IN  WAS COMPLtTEH  IU JUME.
    
    
    
    
    
    
    
    
    
    AUG. 77     THE ARMS  BHOnE OFF  IN THE £5-FOOT U1AMF..TER THICKENLR  TANK,  CAUblNfi A 3U DAYS DOWNTIME.
    
    
    
    
    Sgp. 77     A MAKE-UP nATER BOOSTER PUMP HAD Tli  bF FJEPLACED.
    
    
    
    
    OCT. 77     THE MOTOR DRIVE ON  THE SLAKE.R BELT  HAD Tu BE  REPAIRED.  ALTHOUGH THE SLAKF.R IS NO LDNGtR
    
    
    
    
    USED WITH THE LIMESTONE  REAGENT, THE BELT  IS USED  TO  CONVEY IHt LIMFSTONE  TO THE DISSOLVING TANK.
    
    
    
    
    
    
    
    
    
    1ST UUARTER-1978     IT WAS DISCOVERED 1HAT  wlTh  A  &TUICH10METR1C  RATIO OF  0.75 THE  KfcUuIRED oEGMhE
    
    
    
    
    UF SO?. REMOVAL CAN BE ACHIEVED.  THE CURRENT REGULATION  LIMITS EMISSIONS Tu  ->.d  LBS/MM  OTU HtA I
    
    
    
    
    INPUT.  DURING THE JANUARY BLIZZARD, SUMt FREE/E-ilP  HRuRLEi-iS  HERE ENCOUNTERED.
    
    
    
    
    DURING JANUARY THE BOILERS OPERATED 744  HOUKb AND  THE EGO SYSTEM  UPERATEU  b9b HOURS YIELDING OPER-
    
    
    
    
    ABILITY AND AVAILABILITY INDEX VALUES UF SOX.   ALL OUKiMTiME rtAb A T f R1 SOT ABLE TO  f REFTZE-UPS DURING
    
    
    
    
    BLIZZARD  CONDITIONS.   DURING FEBRUARY,  THE  BOILERS OPERATED b7i HOURS  AND  THE COwTKOL  SYSTEM OPERA-
    
    
    
    
     TED  16H HOORS.   HOWEVER THE  FGU SYSTEM  WAS  AVAILABLE  Sb)  HuURS.   THEREFORE  THE OPERAblLI'Y INDtX WAS
    
    
    
    
    e!5%  WHILE,  THE  AVAILABILITY WAS 8i%.   THE AbSURBER  LlNEb  ftEivE  TIIArtEu  uUT  FEBRUARY b, BUI DURING
    
    
    
    
    FEBRUARY,  THE  GOVERNOR OF OHIO TEMPORARILY  SHELVED  PuLLUTluN CONTROL REGULATIONS.   THEREFORE THE
    
    
    
    
    FGD  SYSTEM  WAS  NOT OPERATED  ALTHOUGH  II  ftAS AVAlLABLt FOK OPERATION.   THE  SYSTEM WAS  SHUIDUWN UN
    
    
    
    
    FEBRUARY  13 AND  DID N01 OPERATE DURING  MARCH.
    
    
    
    
    
    
    
    
    
     £Nu  utlARTER-1978   SYSTEM wAb RESTARTED APRIL  10 AIMF> ^AS REPORTED TO HAVh  RUi-J rtl TH luu% UPF.RA-
    
    
    
    
     blLIlY  INDEX  VALUE FOR  THE REMAINING  PtKIOD.   F'LANl  REPOklfcll  THAI ALL  PRcVlOUS PROULLMS HAVE
    
    
    
    
     bEt.N CORRECTED.   DURING IHE  LAST  PURTJuN OF I Hi. eNU  JUARIE'R 1 Ht  BOILER LOAD DKUPPED fU  T IS SUMMER
    
    
    
    
     LEVEL,  ABOUT  30  MM STU/HR,  AS OPPOSED  10 THE  MAXIMUM COLO SEASi.N  LOAD  OF IbO I'M  HTU/HR.
    

    -------
                                                                                        STATUS  AS  OF  07/30/7a
                                           SECTION  9  (CONTINUED)
                     PERFORMANCE DESCRIPTION KIR OPERATIONAL FGU brsiEMS UN  INDUSIRIAL  BORERS
       INSTALLATION NAME
       INSTALLATION LOCATION
       SOURCE CHARACTERISTICS
       SOURCE RATING
       NUMBER OF  SEPARATE FGD UNITS
       SOURCE CAPACITY
       CONTROL SYSTEM VENDOR
       CONTROL PROCESS
       NEW  /  RETROFIT
       START-UP DATE
       CONTROL SYSTEM STATUS
       SOti  EFFICIENCY
       PARTICULATE  EFFICIENCY
       SLUDGE  OK  BY-PROOUCT  DISPOSAL
    SHELLER GLOBE CORP.
    NORFOLK, VIRGINIA
    COAL  CLESS THAN  u SULFUR)
    6,000 SCFM (TOTAL - tL bOILERS)
     1
    4 hW  (EQUIVALENT); TOTAL - 2 BOILERS
    W.K.  SLY MANUFACTURING CO.
    SODIUM HYDROXIDE SCRUBBING
    RETROFIT
    1975
    OPERATIONAL
    NOT DETERMINED
    NOT DETERMINED
    OVERFLOW TO SEWER/SLUDGE TO LANDFILL
                                            BACKGROUND  INFORMATION
          IN NORFOLK, VIRGINIA, SHELLtR GLOBt CORPORATION  OPERATES  THE  MITCHELL  SMITH  DIVISION PLANT,
    WHERE THE PRIMARY PRODUCT  IS CORK RUBBER GASKET MATERIAL.   PROCESS (AUTOCLAVE)  AND HEATING STEAM
    ARE SUPPLIED BY A BOILER RATED AT 350 BOILER  HP  (ABOUT  3.5  MW  EQUIVALENT).   STEAM CONDITIONS ARE
    125 PSI AT 325 F.  THE BOILER WAS ORIGINALLY  ERECTED  IN  1939,  BUT  UNDERWENT  A  COMPLETE  OVERHAUL IN
    1977.  BOILER TUBES, REFRACTORY BRICK,  GRATE,  AND  SOOT  BLOWERS  WERE  REPLACED DURING THE OVERHAUL.
    THE BOILER FIRES COAL SUPPLIED BY GENERAL COAL - NOMINAL SIZE  IS 1.2b  X  0.25 INCHES.  COAL
    CHARACTERISTICS ARE AS FOLLOWS.  HHV=li,200 faTU/LB, ASH=6X,  ANU SULFUR  IS LESS  THAN IX.
         THE EMISSIONS CONTROL SYSTEM AT SHELLER  GLOBE CONSISTS  OF  A W.W.  SLY WINJET SCRUBBER
    WHICH REMOVES PARTICULATE AND S02 FROM  THE FLUE GAS.  THE SYSTfcM USES  A  SODIUM  HYDROXIDE  MAKE-UP
    FOR SOd CONTROL.  RECYCLE TANK SUPERNATANT IS FH NEUTRALIZED AMD IS  DISCHARGED  To CITY  StWERS.
    FLYASH AND SEDIMEN]  ARE SUMPEO OUT AND  HAULED 10 A SANITARY  LANDFILL.
                                             OPERATING HISTORY
    2ND UUARTER-J978    DURING THE REPORT PERIOD THE UNIT UNDER WENT A VIRGINIA EPA CERTIFICATION
    INSPECTION, AND WAS FOUND TO BE IN COMPLIANCE.  NO SCRUBBER-RELATED PROBLEMS HAVE OCCURRED.
    

    -------
                                                                                      STATUS AS OF 07/it.)/7tt
    
                                          SECTION   «  (CONTlNUfO)
                    PERFORMANCE  DESCRIPTION  FOR  UPt RAT KmAL  FGu SYSTEMS ON INDUSTRIAL BOILERS
      INSTALLATION  NAME
      INSTALLATION  LOCATION
      SOURCE  CHARACTERISTICS
      SOURCE  MATING
      NUMBER  OF  SEPARATE  FbO UNITS
      SOURCE  CAPACITY
      CONTROL SYSTEM VENDOR
      CONTROL PROCESS
      NEW /  RETROFIT
      START-OP DATE
      CONTROL SYSTEM STATUS
      bOd EFFICIENCY
      PASTICJLATfc EFFICIENCY
      WATER  MAKE-UP
      SLUDGE OR BY-PRODUCT DISPOSAL
    
    
      CONTROL SYSTEM COST
    ST. REGIS PAPER LO.
    LANTuNMENT, FLORIDA
    rtAhK AM) GAS OK OIL UESS THAN U SULFURJ
    lib,000 SCFM (1 bOILhHJ
     1
    60 Mh (EQUIVALENT); DESIGN - 300,000 LB/HK STEAM
    AIKPOL INDUSTRIES
    LAUS1IL SCRUBBING
    RETROFIT
    1973
    OPERATIONAL
    80* - SOJi
    94.5X 1400 LB/HR  AT INLET)
    OPtN LOOP; 300 GPM-250 GPM SCRUBBING LIHUOK  FEED
    WASTfcWATtK TREATMENT
    EFFLUEixiT IS TRtATEO IN AN ON-SITE  SEWAGE  TREATMENT  PLANT
    CAPITAL: sioo.ooo  (I97i).  COST  is  FOR  ABSORBER  ONLY.
                                           BACKGROUND INFORMATION
        THE SCRUBBER SYSTEM AT SI. REGIS PAPER LOCATED AT CANTONMENT, FLORIDA  «AS  MANUFACTURED  HY
    AlRPOL.  THE UNIT IS CONSTRUCTED OF JlfaL STAINLESS SIFKL AND HANDLES  A  TOTAL FLOE  GAS  VOLUME  OF
    175,000 ACFM.  PARTICIPATES ARE CONTROLLED WITH CYCLONES PRECEEDING  THE  SCRUBBER.   SCRUBBER PRESSURE
    OROH Is APPROXIMATELY 10 INCHFS rt.G. *vlTH bO TO 90X SULFUR DIOXIDE REMOVAL EFFICIENCY.   THE SCRUBBER
    IS FOLLOWED BY A CHEVEkON-TYPE M1SI ELIMINATOR.
        THt dOILtR IS RATED AT h(l MW AND PRODUCES 300,000 LBS/HR STEAM.   THE TYPICAL  SULFUR  CONTENT
    OF THF FUEL IOIL OR BAKK, NATURAL UAS  TS LESS THAN 1%.
        SCRUBBER UNDERFLOW CONSISTS OF ASH AND A SODIUM SULF1TE/SULFATE  SOLUTION.   THE SLUDGE IS  OIS-.
    CHARdEU TO AN ON-SITE SEftAUE TRFATMENT PLANT.
    
                                             OPERATING HISTORY
    IKi) ijMARTER-1977    KiOUP FIBERS FROM BARK WERE CLOGGiNli  SEPARATORS AND  CONTROL VALVES.   INSPECTION
    BIAS tiAue AND SOLUTION 10 PROBLEM is BEING INVESTIGATED.
    
    4Tn ullARTER-1977    AFtER INVESTIGATION OF THE CLOGGING  PROBLEM  IT WAS  DECIDED TO  CHANGE THE  MAKE-UP
    UP WATER SOURCE.  WATER is NOW OBTAINED FROM A CLEANER PORTION OF  THE PROCESS  LOOP.
    PLAiil RbPOkTS SATISFACTORY OPERATTuNS WITH NO OTHER MAJOR PROBLEMS.
        UMARTER-197B
                        PLUGGING DUE TO FTnERS  I Iv  THE  SCRUBBER  FEEDrtAIER REMAINED TO BE AN UNRESOLVED
    

    -------
                                                                                      STATUS  AS  OF  07/30/78
    
    
    
                                          SECTION  9 (CONTINUED)
    
    
    
    
                    PERFORMANCE DESCRIPTION FOR OPERATIONAL FGO SY5TEMS UN  INDUSTRIAL BOILERS
    
    
    
    ST. RESIS PAPER CO.; CANTONMENT, FLORIDA (CONTINUED)
    
    
    
    
    
    
    PROBLEM DURING THE REPORT PERIOD.  PLANT HAD NOT YET CHANGED THE SCRUBBER LIUUUR FEED SOURCE.   IN
    
    
    
    
    THE JANUARY THROUGH MAY PERIOD, THE BOILER OPERATED 3473 HOURS.  SCRUBBER RELIABILITY INDEX  WAS  NEAR
    
    
    
    
    100 X.  THE PLANT INDICATED THAT THIS REPORT HAD BEEN REPORTING TOO HIGH OF A SULFUR CONTENT IN  THE
    
    
    
    FUEL (2-3 X),  AS COMPARED TO THE CORRECT VALUE OF LESS THAN IX.
                                                    SO
    

    -------
                                                                                       STATUS AS OF 07/30/7d
    
    
    
    
    
                                          SECTION  <>  (cnuTiNUEi))
    
    
    
    
                    PERFORMANCE DESCRIPTION FOR OPERATIONAL  FKI)  SYSTEMS  UN  INfliiSlRIAL d'HLERS
      INSTALLATION NAME
    
    
    
    
      INSTALLATION LOCATION
    
    
    
    
      SOURCE CHARACTERISTICS
    
    
    
    
      SOURCE RATING
      NUMBER OF SEPARATE FGO UNITS
    
    
    
    
      SOURCE CAPACITY
    
    
    
    
      CONTROL SYSTEM VENDOR
    
    
    
    
      CONTROL PROCESS
    
    
    
    
      NFrt / RETROFIT
    
    
    
    
      START-UP DATE
    
    
    
    
      CONTROL SYSTEM STATUS
    
    
    
    
      SOd EFFICIENCY
    
    
    
    
      SLUDGE OR BY-PRODUCT DISPOSAL
    IF.XACO INCuRPORAIED
    
    
    
    SAN AHDO, CALIfORNIA
    
    
    
    OIL 11 .7* SULFUR)
    
    
    
    ihhfOOU SCFM  (TOTAL. - da  HUILERSJ
    
    
    
    dh,000 ACFM n oOOF, FO* EACH  OF  d£ FGO SYSTEMS
    
    
    
    00,000 ALFH a) bOUF, FOR tACH  OF  d  FGD SYSTEMS
    
    
    
    
    d<(
    
    
    
    140 MW (EQUIVALENT);  14&0 MM  BTU/HH:  TOATL - it BOILERS
    
    
    
    
    CFILIOTF;
    
    
    
    SODIUM HYDROXIDE  SCRUBBING
    
    
    
    RETROFIT
    
    
    
    NOVEMBER, 1973
    
    
    
    OPERATIONAL
    
    
    
    73% 11000 PPM o)  INLET)
    
    
    
    wASTtwATtR TKFATMEMT
    
    
    
    HALF  OF  1HE SCRUBBER  UNDERFLOW IS  TREATED AND RECYCLED AS
    
    
    
    BOILER FEF.DWATER;  THL OTHEK HALF' GOES TO WASfErtATER
    
    
    
    DISPOSAL WELLS.
                                            BACKGROUND INFORMATION
    
    
    
    
        TEXACO USES SEVERAL OIL FIRED BOILKftS  AT  ThE  SAN ARDU, CALIFORNIA SITE.   THE  STEAM  IS  INJECTED
    
    
    
    
    IN OIL WELLS TU FACILITATE OIL FLOW.   THERt  ARt  TWu DIFFERENT SIZES l»F THE BOTLEWS:  180  MM ti TU/HR
    
    
    
    
    (2 NOS), AND 50 MM BTU/HK  131 NOS) .   THF FUEL OIL HAS A TYPICAL SULFUR CONTF.iMT  OF  1.7*.
    
    
    
    
        THE FLUE GASES (BO,000 AND db.OOO  ACFM FROh  EACH BuTLErf b) bOo F) ARE SCRUHtSED  BY  A  FGO SYSTEM
    
    
    
    
    SUPPLIED BY CE1LCOTE COMPANY  IN  NOV.  '73.   EACH  riOILER TS FOLLOWED HY A UUENCHIIMG  CHAMBER  ANi) A
    
    
    
    
    SCwUBBER.  THE StRUBbEkS,  WHICH  ARE  HORZONIAL lOrtFRS PACKED wIlH 2 IN. TELLEKAFE  PACKINGS  ARe OF
    
    
    
    
    SIZES:  15 FI X 15 FT X 2(1 FT  IE NUS) ,  AND 15 FT  X t5 FT X 9 I/a FT  (2
    -------
                                                                                         STATUS AS UF 07/30/78
                                            SECTION  '» (i;(JNTINUElJ)
                     PERFORMANCE  UESCKlPTiUN Hh< UPtkAT lUWAL hG.l SYilTtMS  ON  INDUSl«IAu  BOILERS
     fFAALO IrfCOKHUkAlfcu; S«N  ARPU,  CALIFORNIA  ICU.M I tNUfcD J
                                               OPEKA1 I Mi HIS fORY
     IHt  MAJOR  OPERATIONAL PROBLEM AREAS  ARb:
        1.  THfc  UUENCHER SkCUON HAS SUFFERED SEVF.KE  CORROblurj DUE Tu ACID ATTACK.
        ?.  F^P  LINEK OETfklUATES DUE  10 MECHANICAL  ABrtASION n.WING LLtANING OHErtAFIONS.   IT  NEEOS
           OCCASIONAL RESURFACING.
        3.  THE. PACKED BEOS AKE FrttOUENTLY PLUGGED «r HLYASH.   THE OIL TN THE NAf.lHAL LIQUOR  HAS  CAUSED
       FullLINR OF  THE PALKEO BEDS.
    
       «.  OCCASIONAL OVERTNJECTION OF CAUSTIC HAS RESOLTEH IN PLUGGING OK SPRAY NOZZLES  dY  SCALES.
    
    
     !ST gUARIEH-1978    DUE  10 THE LOW S02 REMOVAL AND  HIGH  MAINTENANCE COST OF THE ABOVE DESIGN,  TEXACO
     HAS UNDERTAKEN  A TEST  PROGRAM t,HICH,  IF SUCCESFUL,  MLL  PHASE  UUT  THE PRESENT SCRUBBERS BY  THE  END
     OF 1,79.   FOR MORE  INFORMATION ON THfc PROGRAM SEE  THE  OTHEK  TEXACO,  SAN ARDO BACKGROUND INFORMATION
    tNTWY  IN SECTION 10  OF  THIS  REPORT.
    
    
    MO yUARTER-1978    THE  AVAILABILITY  OF EACH FGD SYSTEM  MAS  APPROXIMATELY  S4 X.   ON AN AVERAGE, ONE
    SYSTfcM WAS SHUTDOWN  1 rtil  DAYS  A MONTH  FOR  HA INTtNANCF.
                                                    If.
    

    -------
                                                                                       STATUS  AS OF 07/30/7B
    
    
    
    
                                          SECTION  9 (CONTINUED!
    
    
    
    
                    PERFuRMANCE DESCRIPTION KOR OPERATIONAL FGJ SYSTEMS UN  INOOSIRIAL  BOILERS
      INSTALLATION NAMt
    
    
    
    
      INSTALLATION LOCATION
    
    
    
    
      bOuRCE CHARACTERISTICS
    
    
    
    
      SOURCE RATING
    
    
    
    
    
    
    
    
      NUMBER OF SEPARATE FGO UNITS
    
    
    
    
      SOORCE CAPACITY
    
    
    
    
      CONTROL SYSTEM VENDOR
    
    
    
    
      CONTROL PROCESS
    
    
    
    
      NEft / RETROFIT
    
    
    
    
      START-UP DATE
    
    
    
    
      CONTROL SYSTEM STATUS
    
    
    
    
      SOi! EFFICIENCY
    
    
    
    
      PARTICULATE EFFICIENCY
    
    
    
    
      SLUDGE OK bY-PROOUCT DISPOSAL
    TEXASGULF
    
    
    
    
    GRANGER, WYOMING
    
    
    
    
    OIL 11.IX SULFUR)
    
    
    
    
    140,000 SCFM (TOTAL - 
    -------
                                                                                       •STATUS  AS  OF  07/i0/78
    
    
    
                                           SECTION  Q (CONT1NUFD)
    
    
    
    
                     PERFORMANCE DESCRIPTION FOR OPERATIONAL FGU SYSTEMS UN INDUSTRIAL TOILERS
    
    
    
     TEXASGULF?  GRANGER,  WYOMING (CUNT INUEO)
    
    
    
    
    
    
    
         EACH  ABSOR6FR  IS DIVIDED VERTICALLY INTO TWO SECTIONS, ONE OF WHICH HAS A DAMPER AI  THE  TOP.
    
    
    
    
     THIS  PERMITS  CURTAILMENT  OF GAS  FLOW THROUGH HALF  OF THE UNITS AT LOW LOADS.  THE ABSORBER,
    
    
    
    
     THEREFORE,  CAN  OPERATE  AT THE  DESIGN EFFICIENCY  rtHLN THE BuILEK PRODUCES FKU« *5l 10 luOX OF US
    
    
    
    
     RATED OUTPUT.   THE ABSORBER BYPASS  ALLOWS  UPTO 25%  OF THE INCOMING HOT FLUE GAS 10 BE DIVERTED.
    
    
    
    
     TYPICALLY,  TtXASGULF USES THE  BYPASS TO KEEP THE FL.Jt GAo IN THE STACK 10 F rtArtMEK THAN  fHAT AT  THE
    
    
    
    
     SCRUBBY  OUTLET.   THE SCRUBBERS  ARE  MADE OF 31b  L  SS, THE TKAYS ARE UOOEHULM 904-L,  THC POMP TANKS
    
    
    
    
     ARE FRP AND THE  STACK i7.5  FT  ID  X  1 bO  FT  HIGH)  IS  OUUbLE-rtALL. INSULATE,, STEEL TYPE «ITH FLAKtLINE
    
    
    
     COATING 6Y  CEILCOTE  COMPANY.
    
    
    
    
    
    
    
    
    
    
                                             OPERATING  HISTORY
    
    
    
    
     1ST QUAKTER-1978     THE OUTLET DUCTWORK, WHICH  IS CORRODED DOE  TO ACID COMPENSATE,  WILL BE REPLACED.
    
    
    
    
     THE SYSTEM OPERATED  WITHOUT  ANY MAJOR PROBLEMS.
    
    
    
    
    
    
    
    
    -------
                                                                                      STATUS  A3  Or  07/3U/78
                                                SEC U DIM 10
    
    
    
    
                   DESIGN  INFORMATION FOR uNDtK LUuSIRUCIION FGI) SYSTEMS UN  INUUSUIAL
      INSTALLATIUN NAME
    
    
    
    
      INSTALLATION LOCATION
    
    
    
    
      SOURCE CHARACTERISTICS
    
    
    
    
      SOURCE RATING
    
    
    
    
    
    
    
    
      NUMBER OF SEPARATE FED UNITS
    
    
    
    
      SOURCE CAPACITY
    
    
    
    
      CONTROL SYSTEM VENDOR
    
    
    
    
      CONTROL PROCESS
    
    
    
    
      NEW / RETROFIT
    
    
    
    
      START-UP DATt
    
    
    
    
      CONTROL SYSTEM STATUS
    
    
    
    
      802 EFFICIENCY
    
    
    
    
      SLUOUE OR BY-PRODUCT DISPOSAL
    CATEkPILLAK fRACIOR CU.
    
    
    
    
    MAPLtfUN, ILLINOIS
    
    
    
    
    CUAL (i.
    -------
                                                                                          STATUS AS  UF  07/iU/7a
                                           oH. ITOlM  in  (COuT ir.ijKu)
    
    
    
    
                   OKSIGN INFORMATION  FUK ,,N,»K LON-S IKUC UN* K(,l, SVSIfHS  0* INDUSTRIAL
     INSTALLATION  NAME
    
    
    
    
     INSTALLATION  LUCATJlMj
    
    
    
    
     SIHJWCF CHARACTERISTICS
    
    
    
    
     SOURCE. RATING
    
    
    
    
    
    
    
    
    
     iJUKHER OF SEPARATE  F(,[) UNITS
    
    
    
    
     SduwCF CAPAClIr
    
    
    
    
    
    
    
    
    
     UONTHflL SYSTEM VENuflK
    
    
    
    
     CB^TKOL PHuCh.SS
    
    
    
    
     ME«  /  KETRUFIT
    
    
    
    
     START-uP  DATE
    
    
    
    
     COiviTHOL SYSTEM STATUS
    
    
    
    
     Sn<:  tft- ICItNCY
    
    
    
    
     SLunGt  OK  dY-pRODUcT DISPOSAL
    
    
    
    
    COAiTwOU SYSTEM CuST
     1>F1 i Y U1L LOMPAMY
    
    
    
    
     bAKEKSHcl.u,  CALIFUHUIA
    
    
    
    
     LRUDfc JIU U.l*  SiJLFuRJ
    
    
    
    
     'i^.S./'^u oC.t-H  (KUAL-/!? BUTLERS)
    
    
    
    
     y  FGU SYSTEMS, EACH  THtAriMG 300,000  ACFM a) 500  F
    
    
    
     9
    
    
    
    
    
     360U  MM itTU/HR,  310-Mrt EQUIVALENT  CTOTAL-7£ BOILERS)
    
    
    
    
     LALH  HillLEH  KAiEU  AT  '43,000 L3S/HR  SfEAM
    
    
    
    
     PRuPKTATARr  iJtSIbN
    
    
    
    
     SiHHUM CAKbOHA Tf SCKUBI3ING
    
    
    
    
     KFTRUFJT
    
    
    
    
     UFCFMBEK,  1^78
    
    
    
    
     CUNSTKUCTTUM
    
    
    
    
     ">h* I  10 PPM SUc? AT OUTLET J
    
    
    
    
     wASTlrWATtW  THHATi-it.NT  AfMD  DISCHARGE  TO  TAILINGS POMU
    
    
    
    
     LAPITAL:  s 500,000 (19/8)  FOR  LACH  SYSTEM.  THIS INCLUDES
    
    
    
    
    COST (IF  SCKUHHEM.SUUA  ASH  T AlMK , PIPING, AND  PUMPS. THE COST
    
    
    
    
    DOES NOT  INCLUDE  STACK, DUCTWORK,  OVERHEADS,  AND ENGINEERING
                                                                   hTo  OR » SJJO.OOO/YK  FOR EACH SYSTEM.
    
    
    
                                              THIS  1,'i  nASF.u ON 340 HAYS/YR. 1 HE COST  I.MCLUuES ELECTRICAL,
    
    
    
                                              SCKUhBtR  MAINTENANCE, AND  SODA ASH.
    

    -------
                                                                                     STATUS  AS OF  07/30/78
                                        SECTillN 10 (CONTINUED)
                 DESIGN INFORMATION FDR UNDER CONS IHUC1 ION Flil) SY.STFMS  ON  INDUSTRIAL BOILERS
    INSTALLATION NAME
    INSTALLATION LOCATION
    SOURCE CHARACTERISTICS
    SOURCE RATING
    
    NUMBER OF SEPARATE F6D ONITS
            SYbTtM UENDOk
            PROCESS
    iMEA / RETROFIT
    START-UP DATE
    COwTHUL SYSTEM STATOS
    S0£ tFFICIENCY
    SLJDGF OR BY-PRODUCT DISPOSAL
    GREAT WESTERN SUGAR
    FRtEMONT.OrllO
    COAL (iX SULFUR)
    40.0UO SCFM a) 70 F  (TOTAL  -  I  BOILERS)
    140,000 LB/HK STEAM  (TUTAL - 2 BOIuERS)
     a
    GREAT WESTERN SUGAR
    SODIUM CARbONATE SCRUBBING
    KETROFIT
    OCTOBER, 1978
    CONSIRUCrluN
    
    WASTEWATER  TREATMENT AND DISCHARGE TO CITY SEWER
                                                    97
    

    -------
                                                                                      STATUS  A3 OF  07/30/78
    
    
    
                                         SECTION 10 (CONTINUED)
    
    
    
    
                  DESIGN INFORMATION FOR UNDER CONSTRUCTION FGD SYSTEMS UN  INDUSTRIAL  BOILERS
     INSTALLATION NAME
    
    
    
    
     INSTALLATION LOCATION
    
    
    
    
     SOURCE  CHARACTERISTICS
    
    
    
    
     SOURCE  RATING
    
    
    
    
    
    
    
    
    
     NUMBER  OF SEPARATE  F6D  UNITS
    
    
    
    
     SOURCE  CAPACITY
    
    
    
    
     CONTROL SYSTEM VENDOR
    
    
    
    
     CONTROL PROCESS
    
    
    
    
     nEw / RETROFIT
    
    
    
    
     START-UP DATE
    
    
    
    
     CONTROL SYSTEM STATUS
    
    
    
    
     S02 EFFICIENCY
    
    
    
    
    WATER MAKE-UP
    
    
    
    
    SLUDGE OR BY-PRODUCT  DISPOSAL
    
    
    
    
    
    
    
    
    CONTROL SYSTEM COST
     MOBIL  OIL  COMPANY
    
    
    
    
     BUI TuNhiLLow,  CALII-OKNIA
    
    
    
    
     OIL  11.IX  SULFURJ
    
    
    
    
     42,000  3UFI»i  (TOTAL  -  T  BUTLFRS)
    
    
    
    
     I FGU  SYSTEMS,  FACH  TREATING  U,<400 ACFM ,OOO us78).   THIS COOT  I.MCLUUES  ABSORBER
    
    
    
    
    MODULES, RECYCLE TANKS,   STACK, DEMISTExS,  PUMPS,  AND  PIPING.
    
    
    
    
     IT  OuEb NOT INCLUDE CAUSTIC TANK, FEED PUMPS,  UR  FfcEO PIPES.
                                         BACKGROUND  INFORMATION
    
    
    
    
      MOBIL OIL HAS PURCHASED SEVEN HEATER TECHNOLOGY EDUCTOR  bCKUWHER  SYSTEMS  FUR THE CONTRUL OF SOd.
    

    -------
                                                                                      STATUS  AS  OF  07/30/78
    
    
    
    
    
                                         SECTION  10  (CONTINUED)
    
    
    
    
                  DESIGN INFORMATION FOR UNoER CONSTRUCTION  FGD  SYSTEMS  ON  INDUSTRIAL BOILERS
      INSTALLATION NAME
    
    
    
    
      INSTALLATION LOCATION
    
    
    
    
      SOURCE  CHARACTERISTICS
    
    
    
    
      SOURCE  RATING
    
    
    
    
      NUMBER  OF  SEPARATE  FGD  UNITS
    
    
    
    
      SOURCE  CAPACITY
    
    
    
    
      CONTROL SYSTEM  VENDOR
    
    
    
    
      CONTROL PRUCtSS
    
    
    
    
      NEW  / RETROFIT
    
    
    
    
      START-UP DATE
    
    
    
    
      CONTROL SYSTEM  STATUS
    
    
    
    
      S02  EFFICIENCY
    
    
    
    
      SLUDGE  OR BY-PRODUCT DISPOSAL
    
    
    
    
      CONTROL SYSTEM  COST
    ST. JOE ZINC co.
    
    
    
    
    MONACA, PENNSYLVANIA
    
    
    
    
    COAL C2.5%-«.5% SULFUR)
    
    
    
    
    104,000 SCFM (TOTAL -  1 BOILER)
    
    
    
    
     1
    
    
    
    
    bO MW  (MINIMAL PEAK CAPACITY)
    
    
    
    
    BUREAU OF MINES
    
    
    
    
    CITRATfc PROCESS
    
    
    
    
    RETROFIT
    
    
    
    
    OCTOBER, 1
    -------
                                                                                        STATUS A3 UF 07/i(»/7a
                     DESIGN  INFORMATION  KIR
    
       INSTALLATION  NAMfc
       INSTALLATION  LOCATION
       SOURCE CHARACTERISTICS
       SOURCE RATING
    
       NUMBER OF SFPARATE FGD UNITS
       SOURCE CAPACITY
       CONTROL SYSTEM VENDOR
       CONTROL PROCESS
       IM£» / RETROFIT
       START-UP DATE
       CONTROL SYSTEM STATUS
       S02 EFFICIENCY
       SLUDGE  OR  BY-PRODUCT  DISPOSAL
       li<  10  (CII..T1IHIED)
    •ER tONSIKJCtluN  FliD  SYSTEMS  ON INDUSTRIAL BOILERS
    
     TEXALO  INCORPORATED
     SAN  ARDO, CALIFORNIA
     UlL  (1.7* SULFUR)
     11/,OOU SCHM  CTOIAL -  9  BOILERS)
     26,000  »LFM 00 F, FUR EACH  UF  9  BOILERS.
      3
     50 MW (EQUIVALENT); bO MM BTU/HR/BOILER
     DUCON COMPANY
     SODIUM CARBONATE SCRUBBING
     REIROFIT
     MARCH, 1979
     CONSTRUCTION
     95%  (1000  PPM g) INLET)
     SCRUBBtR EFFLUENT DISPOSED OF IN WASTE rtELLS
                                            BACKGROUND INFORMATION
        TEXACO  IS  PLANNING  TO  PHASE  OUT  THE EXISTING FGD SYSTEMS AT THE SAN ARUO OIL FACILITY.  AS  THE
    FIRST oTEP  OF  THE  PROGRAM,  9  OF  THE  PRESENT 35 SCRUBBERS ON THE 50 MM BTU/HR STEAM GENERATORS ARE
    BEING REPLACED  BY  A  NEW  SYSTEM.
    
        THE NEK F6D  SYSTEM  IS  BEING  SUPPLIED  BY DUCON COMPANY AND .ILL BE OPERATIONAL «Y MARCH 1979.
    THE SYSTEM CONSISTS  OF THREE  TRAINS  UF  VENTURI  SCRUBBERS AND HORIZONTAL SPRAY TOWERS.  THE FLUE
    GASES FROM 9 STEAM GENERATORS  WILL BE MANIFOLDED INTO  THE SYSTEM (2*4,000  «FM 3 600F).  EACH TRAIN
    CAN TREAT 50% OF THE DhSIGN LOAD  AND CAN  ESt ISOLATED FROM THE FLUE GAS STREAM.  IT  IS HOPED THAT
    THIS SYSTEM DESIGN W1LL  YIELD  SIGNiF1CANTLY HIGHER  AVAUABILITIES' THAN THE DESIGN CURRENTLY IN USE.
    (FOR FURTHER INFORMATION, SEE  THE OTHER TEXACO,  SAN  ARDO,  BACKGROUND  TNFURMAfTON ENTRY IN SECTION 9
    OF THIS REPORT).  THIS SYSTEM  «ILL UTILIZE  A SODIUM  CARBUNATE .ECHNOLOGY FOR S02 REMOVAL.
        THE COMPLETION OF THE PHASE-OUT PROGRAM IS  CONTINGENT  UPON  ME OPERATING SUCCESS OF THE SYSTEM
    AND ANY NOX REGULATIONS WHICH  MAY HE PROMULGATED.
                                                   luo
    

    -------
                                                                                    STATUS A3 OF 07/30/78
    
    
    
    
    
                                              SECTION 11
    
    
    
    
                      UESI6N INFORMATION FOR PLANNED FSD SYSTEMS ON INDUSTRIAL BOILERS
    INSTALLATION NAME
    
    
    
    
    INSTALLATION LOCATION
    
    
    
    
    SOURCE CHARACTERISTICS
    
    
    
    
    SOURCE RATING
    
    
    
    
    
    
    
    
    NUMBER OF SEPARATE FGD UNITS
    
    
    
    
    SOURCE CAPACITY
    
    
    
    
    CONTROL SYSTEM VENDOR
    
    
    
    
    CONTROL PROCESS
    
    
    
    
    NEW / RETROFIT
    
    
    
    
    START-UP DATE
    
    
    
    
    CONTROL SYSTEM STATUS
    
    
    
    
    S0£ EFFICIENCY
    
    
    
    
    PAKTICULATE EFFICIENCY
    
    
    
    
    SLUDGE OR BY-PRODUCT DISPOSAL
    CONTROL SYSTEM COST
    ARCO/POLYMERS, INC.
    
    
    
    
    MONACA, PENNSYLVANIA
    
    
    
    
    COAL (3.OX SULFUR)
    
    
    
    
    236,000 SCFM  (TOTAL - 3 BOILERS)
    
    
    
    
    900rOOO LS/HR STEAM o) 70U PSI6 AND 7DO F.
    
    
    
    
     3
    
    
    
    118 MW  (EQUIVALENT); TOTAL - 3 BOILERS
    
    
    
    
    FMC ENVIRONMENTAL EQUIPMENT
    
    
    
    
    DOUBLE  ALKALI (CONCENTRATED)
    
    
    
    
    RETROFIT
    
    
    
    
    JUNE,  1980
    
    
    
    
    PLANNED-CONTRACT  AWARDED
    
    
    
    
    90*  12,300 PPM a  INLET)
    
    
    
    
    99.5%
    
    
    
    
    DEWA1EREO SLURRY  TO LANDFILL
    
    
    
    
    FLYASH ADDITION TO 0£WfrTER£D CAS03/CA304  FILTER CAKE,
    
    
    
    
    THEN TO LANDFILL.
    
    
    
    
    CAPITAL!  S8i000,000  (1978).  THIS  TOTAL  INSTALLED COST
    
    
    
    
    INCLUDES  EQUIPMENT,  INSTALLATION,  DUCTWORK,  STACK,  PIPING*
    
    
    
    
    COST OF THE  FGO SYSTEM,  ENGINEERING,  START-UP,  AND  TESTING.
    
    
    
    
    INSTRUMENTATION,  ENGINEERING,  AND  OVERHEADS.
                                             OPERATING:  PROJECTED COSTS ARE NOT YET AVAILABLE.
                                                  lot
    

    -------
                                                                                       •STATUS AS UF U7/iO/7«
                                           SECTION 11  (CONTINUEDl
                         DESIGN INFORMATION FOR PLANNED FGO SYSTEMS ON  INDUSTRIAL  BOILERS
       INSTALLATION NAME
       INSTALLATION LOCATION
       SOURCE CHARACTERISTICS
       SOURCE RATING
    
       NUMBER OF  SEPARATE  FGO UNITS
       CONTROL SYSTEM  VENDOR
       CONTROL PROCESS
       NEW  /  RETROFIT
       START-UP DATE
       CONTROL SYSTEM  STATUS
       SOc!  EFFICIENCY
       SLUDGE  OR BY-PRODUCT  DISPOSAL
     C.A.M.lCARHIDE-AMOCO-MONs/ugTU)
     HOUSTON,  TtXAS
     NOT SELECTED
     1,200,000 SCFM  Cl  BOlLERJ
     bOU MW  (EQUIVALENT);  1 BOILER
     1
     NOT SELECTED
     NOT SELECTED
     NEW
     OCTOBER, 1>*8J
     PLANNED-CONSIDERING 802 CONTROL
    NOT DETERMINED
    DISPOSAL TECHNIQUE NOT KNU.i/N
                                           BACKGROUND  INFORMATION
         UNION CARBIDE, AMOCO, AND MUNSANTO HAVE ENTERED  INTO  A  JO!Nr  VENTURE  (C.A.M.),  ,HICH WILL HAVE
    A COGENERATION FACILITY NEAR HOUSTON,TEX AS. THE 60U-MW  (EQUIVALENT)  BOILER  WILL  PRODUCE  ELECTRICITY
    AND PROCESS STEAM FOR THE NEARBY PLANTS UF THE THREE  COMPANIES.
        •HE TYPE OF FUEL TO BE USED IS NOT FINALIZED.  HOWEVER, A FbO SYSTEM  IS  DEFINITELY  BEING
    CONSIDERED. STARTUP FOR THE PO«FR GENERATING FACILITY IS SCHEDULED FUR LATE  1983.
                                                  102
    

    -------
                                                                                       STATUS  48  UF  07/30/78
    
    
    
    
                                          SECTION 11 (CONTINUED)
    
    
    
    
                        DESIGN INFORMATION FUR PLANNED Fbl) SYSTEMS ON  INDUSTRIAL BOILERS
      INSTALLATION NAME
    
    
    
    
      INSTALLATION LOCATION
    
    
    
    
      SOURCE CHARACTERISTICS
    
    
    
    
      SOURCE RATING
    
    
    
    
    
    
    
    
      NUMBER OF SEPARATE FGD UNITS
    
    
    
    
      SOURCE CAPACITY
    
    
    
    
      COi\TROL SYSTEM VENDOR
    
    
    
    
      CONTROL PROCESS
    
    
    
    
      NEW / RETROFIT
    
    
    
    
      START-UP DATE
    
    
    
    
      CONTROL SYSTEM STATUS
    
    
    
    
      S02 EFFICIENCY
    
    
    
    
      SLUDGE OR BY-PRODUCT DISPOSAL
    CARBORUNDUM ABRASIVES
    
    
    
    
    BUFF«LU, NEW YURK
    
    
    
    
    COAL (a1/. S AVERAGE, 3.£% S DESIGN MAX)
    
    
    
    
    38,000 ACFM nl 350 K
    
    
    
    
    60,OUO - 85,000 LBS/HR STEAM  (PROCESS  AND  HEATING  STEAM)
    
    
    
    
     1
    
    
    
    
    10 Mh (EUUIVALENT)
    
    
    
    
    CARBORUNDUM ENVIR. SYS. LTD.
    
    
    
    
    LIME SCRUBBING
    
    
    
    
    RETROFIT
    
    
    
    
    
    
    
    
    
    PLANNED-CONTRACT AWARDED
    
    
    
    
    9251
    
    
    
    
    WASTEWATER TREATMENT AND DISCHARGE  TQ  CITY SEWER
                                           BACKGROUND  INFORMATION
    
    
    
    
       NO DEFINITE PLANS HAVE BEEN MADE FOR THE CONTROL UF SU3 EMISSIONS  FROM THIS  BOILER.   THE FUTURE
    
    
    
    
    OF THE CONTROL SYSTEM WILL BE DETERMINF.D BY A REGULATORY  AGENCY  DECISION  EXPECTED NEAR  THE END OF
    
    
    
    
    1978.  THE CURRENTLY OPERATING VENTURI (1./G = 10)  CONTROLS ONLY  PARTICULATE,  HUT  TIE-INS HAVE BEEN
    
    
    
    
    PROVIDED FOR A LIME SCRUBBING SYSTEM USING A b-STAGF SPRAY TOWER  FOR  S02  CONTROL.
    2ND QUARTER-1978
                                             OPERATING HISTORY
    
    
    
    
                        PLANT REPORTED NO CHANGE.
                                                    10?
    

    -------
    UFSIGN  INFOKMA1
                                                                                         STATUS AS OF  U?/30/7d
                                          oFL TlOlv I 1  CC.ONI IMJFl) )
    
    
    
    
    
                                           FOP  PLANNtO f t,l) SYSrKMS  d,J  INDUSTRIAL
    il»6TALLATJUN N'AME
    
    
    
    
    
              ION LUCATIOI,
    
    
    
    
    
            ChAKACTtKlSHtS
    NlK'.RtR  OF  SFPAKATF Fun  UNITS
    
    
    
    
    •SOuMCE  CAPACITY
    
    
    
    
    COiViTwOL SVbTtM VtMuUK
    NE'f, /  RETROFIT
    
    
    
    
    START-UP  OATt
    
    
    
    
    COKHKOu SYbTtM STA1US
    
    
    
    
    S02 tFflCIENCY
    
    
    
    
    SLUDGE OK  BV-PKODUCT DISPOSAL
                                     U.S.A.  IMC.
    
    
    
    
                                   LLU,  CALIFORNIA
    
    
    
    
                           ulL ll.l/i  bllLFUKJ
    
    
    
    
                           llbiOOO bCFM  (TOTAL - 13 HOTLEr*Sj
    
    
    
    
                           d FGU SYbTtMS,  EACH IHLATIuG  IbU.OOO ACFM a) 500F.
    
    
    
                            2
    
    
    
    
    
                           60U MM 8IU/HK  (TOTAL - Id WOILtRS;  fa HOILEKS/FSI)  SYSTEM)
    
    
    
    
                           IMOI SELtCTtD
    
    
    
    
                           SODIUM CARbOHAlE  SCKOHBING
    
    
    
    
                           RETROFIT
    
    
    
    
                           APRIL/ 147S
    
    
    
    
                           PLANWEU-KEbUESTIUR/EVALUATING BIDS
    
    
    
    
                           SO* IftgO PPM oi  iNLtTj
    
    
    
    
                           nAbTLWATtR TREATMENT
                                                   1 0"4
    

    -------
                                                                                      STATUS AS OF 07/30/78
    
    
    
    
    
                                          SECTION  11  (CONTINUED)
    
    
    
    
                       DESIGN  INFORMATION FOR  PLANNED  FbO  SYSTEMS  ON  INDUSTRIAL BOILERS
      INSTALLATION  NAME
    
    
    
    
      INSTALLATION  LOCATION
    
    
    
    
      SOURCE  CHARACTfcRISTICS
    
    
    
    
      SOURCE  RATING
    
    
    
    
    
    
    
    
      NUMBER  OF  SEPARATE  FGD  UNITS
    
    
    
    
      CONTROL SYSTEM VENDOR
    
    
    
    
      CONTROL PROCESS
    
    
    
    
      NEW  /  RETROFIT
    
    
    
    
      START-UP DATE
    
    
    
    
      CONTROL SYSTEM STATUS
    
    
    
    
      S0£  EFFICIENCY
    
    
    
    
      SLUDGE OR  bY-PROOUCT DISPOSAL
    
    
    
    
      CUNTRQL SYSTEM COS1
    GR1SSOM AIR FORCE BASE
    
    
    
    
    bUNKfcR HILL, INDIANA
    
    
    
    
    COAL (O.SX - 1.6X SULFUR)
    
    
    
    
    33,000 SCFM (TOTAL - 3 BOILERS)
    
    
    
    
    15 Mh  (EQUIVALENT); TOTAL - 3 BOILER.S
    
    
    
    
     1
    
    
    
    
    NOT SELECTED
    
    
    
    
    DOUBLE ALKALI  (CONCENTRATED)
    
    
    
    
    1 NEW  3-HETROF1T
    
    
    
    
    SEPTEMBER,  1979
    
    
    
    
    PLANNEO-KEUUtSTING/EVALUATING BIDS
    
    
    
    
    
    
    
    
    
    DEWATEREU  SLURRY  TO LANDFILL
    
    
    
    
    CAPITAL:  $i,dOo,ooo -  sa,000,000  (1978).   THIS  is  THE
    
    
    
    
    PRUJECTED  TOTAL  INSTALLED  COST.
                                           BACKGROUND INFORMATION
    
    
    
    
        AT GRISSOM AIR FORCE BASE NEAR BUNKEK HILL, INDIANA, THE AIR FORCE HAS  INITIATED  A  PROJECT  WHICH
    
    
    
    
    INCLUDES THE ERECTION OF A NEW COAL-FIRED BOILER AND AN FGO SYSTEM FOR THE  NEW  UNIT AND TWO  EXISTING
    
    
    
    
    COAL-FIRED UNITS.  THE AMOUNT OF CAPITAL ALLOCATED FOR THE EMISSIONS  CONTROL  SYSTEM IS  IN  !H£
    
    
    
    
    $1.8 - $2.0 MILLION RANGE.   THE NAVY IS THE MILITARY CONSTRUCTION AGENT  FOR THE PROJECT.   ARNOLD  M.
    
    
    
    
    DIAMOND HAS THE OVERALL CONSTRUCTION CONTRACT  AND I-OSDICK AND  HILMER  (CINCINNATI)  IS  THE  A-E FIRM
    
    
    
    
    FOR THE FGD PORTION OF THE PROJECT.
    
    
    
    
        THE A-E FIRM HAS SPECIFIED A CONCENTRATED  DOUBLE ALKALI SYSTEM FOR THE  CONTROL APPROACH.  FLUE
    
    
    
    
    GAS FROM EACH BOILER WILL PASS THROUGH A MECHANICAL COLLECTOR.   I HE  GAS  FROM  ALL THREE  8UILERS WILL
    
    
    
    
    THEN Bt MANIFOLDED TOGtTrtER  AND PASS THROUGH ThO PARALLEL ABSORBER TWAINS,  EACH TRAIN CAPABLE OF
    
    
    
    
    HANDLING SOX OF  THE FLUE GAS.  THE MAXIMUM FLOU RATE IS  33,000  SCFM  (145,000  LB/HR OF GAS).
    
    
    
    
        THE BOILERS  FIRE APPROXIMATELY 40% EXCESS  AIR.  COAL MAY RANGE FROM  0.9X  -  4.6% SULFUR AND WILL
    
    
    
    
    HAVE AN AVERAGE  HEATING VALUE OF  11,500 BTU/LB.  THF A-E FIRM  HAS SPECIFIED THAT THE  MAXIMUM 802
    
    
    
    
    OUTLET CONCENTRATION MLL b£  1.2  Lb/MM B1U,  AND THt MAXIMUM PAKUCULATE  AT  THE  OUTLET WILL BE
    
    
    
    
    0.171 Lrt/MM 6TU.
    
    
    
    
        PROJECT COMPLETION  IS SCHEDULED  FOR AUGUST 30,  197B.
                                                    105
    

    -------
                                                                                        STATUS  AS  UF  07/40/7(1
                                                  SECTION  12
                            DESCRIPTION OF INDUSTRIAL  BOILER  FGU  SYSTEMS NOT
       INSTALLATION NAME
       INSTALLATION LOCATION
       SOURCE  CHARACTERISTICS
       SOURCE  RATING
    
       NUMBER  OF  SEPARATE FGD UNITS
       SOURCE  CAPACITY
    
       CONTROL  SYSTEM VENDOR
       CONTROL  PROCESS
       NEW / RETROFIT
       STARI-UP DATE
       CONTROL  SYSTEM STATUS
       SOd EFFICIENCY
       SLUDiiE OR BY-PRODUCT  DISPOSAL
       CONTROL  SYSTEM COS1
     BUNGE,  INC.
     CAIRO,  ILLINOIS
     IOAL  (4%  SULHIR)
     <4<4,000  SCFM  tTOTAL  - ?. BUFLFRS)
     Bl »«i)0  ACFM  at  b2u F
      1
     ill  Mn  (EOUlVAl.tNF) ;  TOIAL - £ HOILtHS
     180,UOU LBS/HP.  STEAM (TOTAL)
     UWAVU tOKP./NAT'L LIME ASS'N
     LIME SLPUBbfNR
     RETROFIT
    
     TERMINATED
     <*«% 13700 PPM INLET)
    UEnATERFLi SLORkY To  LAignFILL
    CAPITAL COST: 4i,ouo,ooo  (is??).   INCLUDES: TOTAL INSTALLED
    COST OF THE FGU SYSTEM, ENGINEERING,  START-UP, Aivil) TtSTIuG.
                                            RACKGKOUNu INFORMATION
        bONGE PORCHASEU THIS LIME  SCRUBBING SYSTEM FOR US! ING PURPOSES.   THE LEvKIS  SCHUdHtR,  WHICH IS
    A HOKIZONT.AL RuTART VESSEL rtUh  IMEkNAL  MAINS,  PFRFORMEl) VEKY >-,LLL DURING  FriE TtSl  t-9
    -------
                                                                                    STATUS  »S  OF  07/30/76
                                        SECTION 12 (CONTINUED)
                         DESCRIPTION OF INDUSTRIAL MOILEK FGD SYbTtMS NO I UPtRATING
    INSTALLATION NAME
    INSTALLATION LOCATION
    SOURCE CHARACTERISTICS
    SOURCE RATING
    NUMBER OF SEPARATE FGD UNITS
    CONTROL SYSTEM VENDOR
    CONTROL PROCESS
    NEW / RETROFIT
    START-UP DATE
    CONTROL SYSTEM STATUS
    502 EFFICIENCY
    SLUDGE OR BY-PRODUCT DISPOSAL
    GRtAI WESTERN SUGAR
    LONGMONT, COLORADO
    COAL C0.7X SULFUR)
    GREAT WESTERN SUGAR
    AMMOMA-LADEN PROCESS WATER
    RETROFIT
    (JCTObER, 1973
    TERMINATED
    351  (300-
    -------
                                                                                         STATUS Ab UF (J7/iO/76
                                            SECTION If. IC
                             DESCRIPTION  (,F  iruuSlKlAL HIM LEU fGL; SYhltMS NO I
       INSTALLATION NAME
       INSTALLATION LOCATION
       buuRCF. CHARACTERISTICS
       bUuRtE RATING
       NUMBtrt OF SEPARATE FbD LIMITS
       SOURCE CAPACITY
       CONTnf>L SYSTEM VENDOR
       COcMTKfiL PROCESS
       iMFrt /  kETRUFIT
       STAR1-UP DATE
       CONTROL SYSTEM STATUS
       SO* tFFICIENCY
       (•ARTICULATE EFFICIEMCY
       SLUDGE OR 8Y-PROUUCT  DISPOSAL
               SYSTEM COST
    HARRIS  MINlNb  LCI.
    SPKULF  PiMfc, NURTH CAROLINA
    COAL  (U.ll%  SULHIM1
    «,ono bl^M  II01AL  - d  HOILERS)
     £
    ii MW  (EUUIVALEnTJ ;  TOTAL  - d HUILEKS
    ft.W.  SLY  MANUFACTURING CU.
    nAIER 5CKUUH1NG  (NArNHi OPTN.)
    RETROF1 I
    l«/3
    1 ERMINATtD
    DISPOSAL TECHN10UE NUT  KNOWN
    CAPITAL: sji.ooo  d9/3j.   THIS  is  rut  TOTAL INSTALLED co
                                            BACKGROUND  INFORMATION
         IHE  F6D  SYSTEM AT  THE HARRIS MIMING COMPANY LOCATED  AT  SPRuCt  PINE,  NORTH CAROLINA REMOVES FLY-
    ASH  ANO  SULFUR  DIOXIDE FROM IHE FLUt GAS OF A COAL FiREH BOILE*.   THE  SCRObBER IS A „.,,. SLY
    IHHluetNT  TYPE  SCROBBER CONSTRUCTED OF 304 SlAINLfcbS 8IEEL.  THE BOILER  IS  RATED 1.9 M*
    ItuHlVALfcNT  ^00  60ILER HORSEPOWER).  COAL COMPOSITION IS TYPICALLY  O.H*  SULFuR AND 5* ASH.  PRIMARY
    INIfKEST IN  FLUE  GAS SCRUBBING IS IN FLYASh REMOVAL AND  NO  TESTS FOR SULFUR DIOXIDE REMOVAL EFFI-
    CIENCY HAVE  BEEN  MADE.
                                              OPERATING HISTORY
    
    -------
                                                                                    STATUS AS OF 07/30/78
                                        SECTION 12 (CONTINUED)
                         DESCRIPTION OF INDUSTRIAL BUILER F6D SYSTEMS NOT OPERATING
    INSTALLATION NAME
    INSTALLATION LOCATION
    SOURCE CHARACTERISTICS
    SOURCE RATING
    NUNBtR OF SEPARATE FGD UNITS
    SOURCE CAPACITY
    
    CONTROL SYSTEM VENDOR
    CONTKOL PROCESS
    NEW / RETROFIT
    START-UP DATE
    CONTROL SYSTEM STATUS
    S0£ EFFICIENCY
    PAKTICULATE EFFICIENCY
    WATER MAKF-UP
    SLUDGE OR BY-PRODUCT DISPOSAL
    QUALITY MILLS, INC.
    MT. AIRY, NORTH CAROLINA
    
    FUEL OIL
    5 MW (EQUIVALENT)* TOTAL - THREE BOILERS
    52,000 Lb/HR STEAM
    COMMERCIAL FABRICATION & MAC
    
    WATER SCRUBBING
    RETROFIT
    
    MAY, 1970
    TERMINATED
    47X  (600-800 PPM 9 INLET)
    60X-95X  (0.05-0.16 GRAIN/SCF a  INLET)
    40 GPM*  OPEN LOOP
    WASTEWATER TREATMENT  AND DISCHARGE  TO  CITY  SEWER
    SCRUBBING LIQUOR DISCHARGED  TO  NEUTRALIZATION  POND
                                                  109
    

    -------
                                                                                      STATUS  AS  l)F  U7/iU/7«
                                         SECTION 12 (CONTINUED)
    
    
    
    
                          DESCRIPTION OF  INDUSTRIAL BOILER FGO SYMEMS Mil OPERATING
     INSTALLATION  NAME
    
    
    
    
     INSTALLATION  LOCATION
    
    
    
    
     SOURCE CHARACTERISlICS
    
    
    
    
     SOURCE RATING
    
    
    
    
     NUMBER OF SEPARATE  FGD  UNITS
    
    
    
    
     SOURCE CAPACITY
    
    
    
    
     CONTROL SYSTEM VENDOR
    
    
    
    
     CONTROL PROCESS
    
    
    
    
     HE*, / RETROFIT
    
    
    
    
     START-UP DATE
    
    
    
    
    CONTROL SYSTEM STATUS
    
    
    
    
    SOd EFFICIENCY
    
    
    
    
    WATER MAKE-UP
    
    
    
    
    SLUDGE OR BY-PRODUCT DISPOSAL
     TRANSCU  TEXTILES,  INL.
    
    
    
    
     AUGUSTA,  GtORGIA
    
    
    
    
     FLItL OIL  (ex MAX.  SULFUR)
    
    
    
    
     50,000 ACFM
    
    
    
    
     0
    
    
    
    
     ao MH
    
    
    
    
     FMC ENVIRONMENTAL  EOUIPMtNl
    
    
    
    
     SOUIUM CARbONAIE SChUBtalNR
    
    
    
    
     NEW
    
    
    
    
     MARCH, 1S75
    
    
    
    
     TERMINATED
    
    
    
    
     80X-65%  tf.10 Lb/HR al INLET)
    
    
    
    
     <4fl GPM* OPtN LOOH
    
    
    
    
    WASTtHATfcR TREATMENT AND DISCHARGE  TO  KIVF.R
    
    
    
    
               LIRuOK DISCHARGED  Tu A HOLDING  POND
                                                 1 1C
    

    -------
                                                                                     STATUS AS OF U7/30/7»
                                        SECTION  12  (CONTINUED)
                         DESCR1PUUN OF INDUSTRIAL  HOILfK  HGD  SYSTtMS  NOT  OPERATING
    INSTALLATION NAME
    INSTALLATION LOCATION
    SOuMCE CHARACTERISTICS
    SOUftCF RATING
    NUi«iBtH OF SEPARATE FGD UNITS
    SOURCE CAPACITY
    COiMTrtOL PROCESS
    NF.w / RETROFIT
    START-OP DATE
    CONTROL SYSTEM STATUS
    SO* tFlFICIENCY
    PAKTJCULATE EFFICIfcNLY
    WATER MAKE-UP
    SLUDGE OR BY-PRODUCT DISPOSAL
    O.b. GYPbUM COKf.
    UAKMON1* PENNSYLVANIA
    C.OAL
    1«»,300 SCFM  (TOTAL  -  1  BOILERS)
    AIRHOL INOOS1R1ES
    UOOBLE ALKALI  (DILUTE)
    NfcW
    
    TtKMlNATEO
    MEETS COUE
    MEETS COUE
    10 GHM*  CLOSED LOOP
    DEWA1ERED  SLURRY  TO LANDFILL
    SLUDGE TO  POND FOR  DHY1NG. THEN TO LANDFILL.
                                                   Ill
    

    -------
             SECTION 13
    
    
    
    
    
    
        PROCESS DIAGRAMS FOR
    
    
    
    
    INDUSTRIAL BOILER FGD SYSTEMS
                    112
    

    -------
                A-l
    Q-
    
    F-l
                                          T-l
    h1
                                                               T-2
                           p-i
                      -A
                      P-2
                                             L—Q-
    
                                                P-3
                                                        RF-1
        FIGURE  13-1.   PROCESS DIAGRAM FOR CATERPILLER TRACTOR,
    
                    JOLIET INDUSTRIAL  BOILER FGD SYSTEM
                                      113
    

    -------
      F-l
                       L,
         T-2
                    P-l
                               T-l
    J
                                       p-1
               P-2
                   T-3
                                                     P-3
    FIGURE 13-2.   PROCESS DIAGRAM FOR GENERAL  MOTORS,
           DAYTON INDUSTRIAL BOILER FGD SYSTEM
                      EQUIPMENT  LIST
    Equipment no.
    A-l
    F-l
    P-l
    P-2
    P-3
    T-l
    T-2
    T-3
    Name
    Absorber
    F.D. fan
    Recirculation
    pump
    Caustic pump
    Bleed off
    pump
    Recycle tank
    Caustic tank
    Bleed off
    tank
    _^____^^_
    Size, feet
    6 diameter x
    35,000 scfm
    200 gpm, 25
    80 gpm
    50 gpm
    7 . 5 diameter
    9 diameter x
    6 diameter x
    10 high
    9 in. WG
    head
    
    
    x 12 high
    18 high
    6. 5 high
    Material of construction
    No.
    316L SS j 2
    Carbon steel
    Carbon steel, rubber -lined
    Carbon steel
    Carbon steel, rubber -lined
    316L SS
    Carbon steel
    316L SS
    2
    3
    1
    2
    1
    1
    1
                              114
    

    -------
    H-l
    — ©— ^
    XNXS^
    /n
    
    
    A-l
    
    
    1
    F-l 	 f.
    J\
    
    — 'i
    c
    
    
    
    
    S-l
    >T" ~T^
    r~! S"V \
    .„, ,_ 	 .^ T_ "t
    *" ' -5 L»* T-4
    n']M ^y^ ^^L^
    ^ P-3 RF-1 T'5 -~l
    •5=4 — -vj- K-
    P-l p.2
    FIGURE 13-3. PROCESS DIAGRAM FOR GENERAL MOTORS,
    PARMA INDUSTRIAL BOILER FGD SYSTEM
    EQUIPMENT LIST
    
    A-l
    F-l
    H-l
    P-l
    P-2
    P-3
    P-4
    P-5
    RF-1
    S-l
    S-2
    T-l
    T-2
    T-3
    T-4
    T-5
    T-6
    Name
    i Size, feet ; Material of construction i No.
    Absorber 10.5 diameter x 22.5 316L SS 4
    high
    F.D. fan 200 hp, 12 in. KG Carbon steel ] 4
    • 4
    Reheater :
    Recirculation Carbon steel, rubber-lined 4
    pump l
    Recirculation |
    pump i
    Underflow pump Carbon steel, rubber-lined 1
    Underflow pump Carbon steel, rubber-lined 1
    1
    Filtrate pump
    Rotary vacuum 500 square feet area Carbon steel, polypropylene 2
    filter : cloth I
    Lime silo . Carbon steel ', 2
    Soda ash silo '. Carbon steel 1
    Chemical mix 5000 gallons Carbon steel 1
    tank j
    Chemical mix 5000 gallons ] Carbon steel 2
    tank
    Clarifier 11 60 diameter x 14 high ' 1
    Clarifier *2 ; 60 diameter x 14 high !
    Filtrate tank ,4 diameter x 7 high ; Carbon steel , 1
    Recirculation Carbon steel, tar coating 4
    tank
    115
    

    -------
                  F-!
                          A-l
    FIGURE 13-4.  PROCESS  DIAGRAM FOR KERR-McGEE,
         TRONA INDUSTRIAL  BOILER FGD SYSTEM
                   EQUIPMENT  LIST
    Equipment no.
    A-l
    F-l
    H-l
    P-l
    T-l
    Name
    Absorber
    F.D. fan
    Reheater
    Recirculation
    pump
    Recirculation
    tank
    Size, feet
    30 diameter x 35 high
    
    50°F reheat
    125 gpm
    
    Ma ter i
    Carbon
    lined
    Carbon
    Carbon
    Carbon
    
    
    steel, fiberglass
    , 316L SS trays
    steel
    steel
    steel, rubber-lined
    
    No.
    2
    2
    2
    2
    2
                           116
    

    -------
      F-l
     T-1
                             A-1
                   Q-l
                                              T-3
                            T-2
    J
                                      P-l
    FIGURE  13-5.   PROCESS DIAGRAM FOR TEXASGULF,
        GRANGER INDUSTRIAL BOILER FGD SYSTEM
                    EQUIPMENT  LIST
    Equipment no.
    A-1
    F-l
    P-l
    
    Q-l
    T-1
    T-2
    T-3
    Name i Size, feet i Material of construction
    Absorber
    15.0 diameter x 20.5 ; 316L SS, trays Inconel 625
    high ;
    F.D. fan ;
    Recirculation 550 gpm >? 15 psig
    pump i
    Quencher
    Liquor head '
    tank
    Recirculation
    tank
    Head tank
    
    
    
    
    
    
    
    
    
    No.
    1
    
    2
    
    1
    1
    1
    1
                             117
    

    -------
      1. REPORT NO.
                                     TECHNICAL REPORT DATA
                               (flease read Instructions on the reverse before completing)
      EPA-600/7-78-052b
                                2.
                                                           3. RECIPIENT'S ACCESSION NO.
      EPA INDUSTRIAL BOILER FGD SURVEY: Second
        Quarter 1978
                                     5. REPORT DATE
                                      July 1978
                                      «. PERFORMING ORGANIZATION CODE
     J. Tuttle, A. Patkar,  N. Gregory, and M. Eckstein
                                                           8. PERFORMING ORGANIZATION REPORT NO
     9. PERFORMING ORGANIZATION NAME AND ADDRESS
     PEDCo. Environmental,  Inc.
     11499 Chester Road
     Cincinnati, Ohio 45246
                                     10. PROGRAM ELEMENT NO
                                     EHE624
                                     11. CONTRACT/GRANT NO.
                                     68-02-2603, Task 36
                         E AND ADDRESS
      EPA, Office of Research and Development
      Industrial Environmental Research Laboratory
      Research Triangle Park, NC  27711
                                     13. TYPE OF REPORT AND PERIOD COVERED
                                     Task Final; 4-6/78
                        ERL-RTP pr°iect
                                     14. SPONSORING AGENCY CODE
    
                                       E PA/600/13
                                 Michael McAdams, Mail Drop 61,
     of flue gas desulfurization (FGD) systems to industrial boilers.  Design and operation
     data has been obtained from 152          FGD control systems, with a capacity of
     8.3 million acfm (2200 MW equivalent). An  average of more than six FGD units
     per year have come on line since 1972,  indicating FGD to be a viable method of con-
     trolling SO2 emissions. The information was obtained by a survey of plant personnel,
     control system vendors, regulatory agencies, and consulting engineering firms. The'
     data is given in two types of tables: one gives summary information; the other, de-
     tailed information. Summary tables present information as a function of control pro-
     cess, control system vendor,  disposal techniques, operation status,  start-up date,
     and flue gas capacity. Detailed information  includes:  control system design, econo-
     mics, operating experience, problems and solutions, waste disposal techniques, and
     maintenance practices.
     7.
                                 KEY WORDS AND DOCUMENT ANALYSIS
                    DESCRIPTORS
                                              b.IDENTIFIERS/OPEN ENDED TERMS
                                                 c. COS AT I Field/Group
     Pollution
     Flue Gases
     Desulfurization
     Boilers
     Waste Disposal
     Maintenance
    Pulping
    Chemical Industry
    Pollution Control
    Stationary Sources
    Industrial Boilers
    13B
    2 IB
    07A,07D
    ISA
    15E
    13H
                STATEMENT
     Unlimited
                                              19. SECURITY CLASS (This Report)
                                              Unclassified
                                                 21. NO. OF PAGES
                                                     124
                                              20. SECURITY CLASS (Thispage)
                                              Unclassified
                                                 22. PRICE
    EPA Form 2320-1 (9-73)
                       118
    

    -------