x>EPA
                                  United States
                                  Environmental Protection
                                  Agency
                                  Municipal Environmental Research
                                  Laboratory
                                  Cincinnati OH 45268
                                  Research and Development
                                  EPA-600/S2-81-102 July 1981
Project Summary
                                  Ferrous  Metals  Recovery at
                                  Recovery  1,   New  Orleans,
                                  Louisiana
                                  Louis P. Soldano
                                   This report summarizes four final
                                  technical reports that document a
                                  series of five tests (referred to as Test
                                  Nos.  4.01, 4.03, 4.05, 4.07, and
                                  4.09) of ferrous metal recovery from
                                  municipal solid waste (MSW) at the
                                  New Orleans, Louisiana, Resource
                                  Recovery Project (Recovery 1). Test
                                  No. 4.01 documented the performance
                                  of the trommel-unders magnetic drum
                                  separator. Test No. 4.03 was conducted
                                  to evaluate the efficiency of shredded
                                  trommel-overs separator. Tests Nos.
                                  4.05, 4.07, and 4.09 were conducted
                                  to evaluate the efficiency and energy
                                  consumption of  a shredder and air
                                  classifier added to the ferrous metal
                                  recovery system. Hammer wear was
                                  also measured for the shredder.
                                   This Project Summary was devel-
                                  oped by EPA's Municipal Environmen-
                                  tal Research Laboratory, Cincinnati,
                                  Ohio, to announce key findings of the
                                  research projects that are fully docu-
                                  mented in separate reports (see Project
                                  Report ordering information at back).

                                  Introduction
                                   This report describes the  ferrous
                                  metal recovery testing done at a full
                                  scale  resource recovery operation at
                                  Recovery I, New Orleans, Louisiana.
                                  Resource recovery of MSW consists of
                                  collecting materials (ferrous metals,
                                  aluminum, glass, paper, etc ) from
                                  processed or unprocessed municipal
                                  refuse. At  Recovery  1,  attempts to
                                  recover ferrous metal were done initially
                                  with a trommel and two drum magnets.
                                  The waste was passed through a trommel
                                  (a large horizontal metal drum perfo-
                                  rated with holes) The  waste falling
                                  through the holes (trommel unders) and
                                  waste passing through the trommel
                                  (trommel overs) was subjected to mag-
                                  nets that recovered any ferrous metal.

                                   Test  No. 4.01  evaluated the belt
                                  magnet performance for recovering
                                  ferrous metal from the trommel under-
                                  flow. Test No 4 03 evaluated the belt
                                  magnet performance on the trommel
                                  overflow.

                                   The contractor for the ferrous metal
                                  required that the product meet the
                                  following criteria: maximum contami-
                                  nation, 4 percent; bulk density, 21.5 to
                                  26.0 Ib/ft3; and shred size, maximum, 5
                                  percent less than 1 in. Since the trommel
                                  and  belt magnets could not produce
                                  materials meeting this  criteria, the
                                  system was modified. Test No. 4.07 was
                                  conducted to evaluate the efficiency of a
                                  hammermill  (shredder) followed by a
                                  belt magnet in liberating and separating
                                  contaminants from the  ferrous metal
                                  recovered from the trommel. The system
                                  was further upgraded to include an air
                                  knife and another belt magnet (Figure
                                  1). Test Nos. 4.05 and 4.09 examined
                                  the modified  system's ability to protect
                                  the shredder from dense objects and
                                  reduce  contamination of the  ferrous
                                  product. This  report describes the results
                                  of the evaluations.

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Test No. 4.01, Trommel-Unders
Magnetic Drum Separator
  At Recovery 1, there are two primary
magnets  The function of the magnets is
to remove  ferrous metal from that
portion of the MSW that has either
passed through the 4-3/4-m.-diameter
circular openings in the trommel or
flowed out the end of the trommel. The
passing material is known as the trommel
underflow and the magnet, the trommel
underflow magnet. The drum magnets
used  are suspended over the head
pulleys of the underflow and'overflow
conveyors
  The trommel underflow magnet is an
electromagnetic type 42 in. in diameter
and 54 in long. The electromagnetic
coil is powered by direct current (DC)
supplied  by a rectifier rated for 5,200
watts  and 230 VDC.
  The most significant size range for the
feed of the trommel is less than 4 in and
greater than 2 in  In the feedstock, on a
clean  metal basis, this size  range ac-
counted for 72  percent of the  magnetic
opportunities by weight
  The magnetically removed ferrous
underflow product is cleaned by sepa-
rating light gauge ferrous  material
(mainly cans) from heavier gauge (non-
can) ferrous materials. Contamination
carried over at the time the ferrous
material was extracted from the waste
stream is pneumatically removed. (The
term "contamination" not only includes
material caught on the ferrous product,
but material actually physically joined to
the product). This section of the report
discusses the efficiency of the trommel
underflow magnet as a light gauge
ferrous separator. The underflow mag-
net showed an  average efficiency of 87
percent measured on  an  "as received"
basis.  Magnetic efficiency on a clean (no
contamination) metal basis for the light
metal  is 92 percent The efficiency of the
underflow magnet in terms  of clean
metal was 85 percent  for the heavy
ferrous metals. Magnetic efficiency was
highest for food cans (98 percent) and
lowest for composite cans (11  percent)
  The magnet itself acts as a cleanup
device, since it differentially attracts
magnetics as  a function of their con-
tamination  As far as composite and
contaminated food cans are concerned,
an object that is less than one-third
magnetic material will probably be ex-
tracted by the magnet.
  According to the test results, for every
100 Ib of trommel underflow magnet
product, 65-1/4 Ib  is the desired light
Raw MSW-
• Trommel	>-Trommo/ overs-
                III
• Shredder •
 Discard
   I
-Belt Magnet
                Trommel Unders
                Air Classifier -
                      Belt Magnet


                     • Cyclones^—
                Aluminum Feed
                      Landfill
           — Ferrous

                 I
            Ferro us	
            Concentrator

                 I
            Light Ferrous
                                                            Heavy Ferrous-^
Figure 1.    Final upgraded ferrous metal recovery system at Recovery 1
gauge  ferrous, 22 to 14 Ib is heavy
ferrous, 2 Ib is loose contamination, 9-
1 /4 Ib is entrapped contamination (light
ferrous), and  1-1/4 Ib  is entrapped
contamination (heavy ferrous)  The
amount of contamination of the light
gauge,  almost  12-1/2 percent, is  un-
acceptable for market use

  Assuming one day's waste of 650
tons, with a bulk density of 16.6 Ib/ft2, ;s
processed at approximately 62 5 tph,
the trommel underflow magnet would
produce 17-1/2 tons of magnetic metal
per day. Just under 13 tons would be the
desired  light ferrous metal. Roughly 4-
1/2 tons would be heavy ferrous  The
magnet would also produce 2 tons of
entrapped contamination and 1 /4 ton of
loose contaminants

  On a  650-ton  MSW day, if perfect
separation of heavy ferrous and loose
organics was accomplished by the
cleanup steps, the shipped material
would  average 2,820 Ib/hr on an  as
received basis.  Of this, 350 Ib/hr would
be entrapped contamination (at 12.4
percent shipped material) This is well
above  the market specification of 4
percent nonmagnetic material.

  The  project  data resulted from  the
average of test runs of 15  sec each at
nominal operating conditions The data
developed from these tests  were  not
extensive enough to differentiate among
the causes of  measured variations in
runs. Some of these variables included
gauss strength, level of ferrous opportu-
nity, composition of feed, and relative
weight  of specific materials.
                         Test No. 4.03, Shredded
                         Trommel-Overs Magnetic
                         Drum Separator
                           Ferrous metal recovery is also prac-
                         ticed on the trommel overflow. Material
                         that does not pass through the trommel
                         holes  is conveyed  to a shredder and
                         reduced to a  nominal 90 percent by
                         weight less than 4 in It then passes J
                         under a rotary drum electromagnet. The*
                         ferrous removed is cleaned up by blow-
                         ing off loose organics and separating
                         the light from the heavy ferrous metals.
                         The magnetic drum separator used was
                         a  Stearns  rotary drum electromagnet,
                         72 in. long and 48 in wide. The shredder
                         is a Heil* shredder
                           The  test on  the  trommel overflow
                         consisted of a number of 10-sec runs at
                         a  nominal rate of 23.5 tph, of which the
                         ferrous component accounted for about
                         7  percent of the total weight The total
                         in-feed mass reporting to the trommel
                         overs is 37.7 percent.
                           Ferrous metal objects in the trommel
                         overflow feed are primarily in one of two
                         categories: tin-plated steel cans that are
                         too large to pass through the trommel
                         holes and smaller cans that fail to report
                         to the  trommel overflow.
                           The  design efficiency of the trommel
                         overs magnet is 95 percent  Test runs
                         showed an average 27  percent effi-
                         ciency. If the data were projected on a
                         clean-metal basis, the magnetics in the
                         trommel overs would comprise 13.5
                         tons of ferrous available for recovery for
                        •Mention of trade names or commercial products
                        does not constitute endorsement or recommenda-
                        tion for use                           \

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ieach 650 tons of MSW. At the measured
efficiency, 2.7  tons  per day would be
recovered and  108 tons per day would
be lost. The principle reason for the low
recovery is that the air gap between the
trommel overs and the magnet belt is 48
percent greater than the design air gap
The  efficiency of the trommel  overs
magnet was also different for the com-
ponent  categories.  The magnet was
more efficient on the light gauge frac-
tion than on the heavy.
  For every 100 Ib of magnetic trommel
overs product (on an "as received"
weight  basis), approximately 61.5 Ib
was light gauge,4.5 Ibwascontammant
attached to  light gauge,  33 5 Ib was
heavy gauge, and 0.5 Ibwascontammant
attached to heavy gauge.
  Seventy-five  percent of the recovered
magnetics (clean-weight basis) were
above 2 in. This size group contained 95
percent of the contaminant found in the
ferrous fraction. The particles greater
than 4 in were contaminated the most.
In all, contaminant accounted for 11
percent of the ferrous fraction. The
recovered magnetics contained 37
percent contamination, on an air dry
basis.
  The samples taken from the trommel
overs feed and the product were tested
for moisture content, bulk density, size
distribution, residual magnetics, and
contamination. It was found that the
product is richer  in  bi-metal cans and
tin-plated steel cans than the feedstock.
Most composite can material in the
feedstock did not report to the  product.
Noncan material is less highly concen-
trated in the product than  in the feed-
stock.


Test No. 4.07, Hammermill
and Belt Addition
  Testing was done on the trommel
overs and unders system  modified by
the addition of a  small hammermill so
that attached or entrapped contaminant
could be freed.  A belt magnet was used
to separate metal from the liberated
contaminant.
  The shredder has four  rows of four
hammers each constructed of maganese
steel with hard facing The belt magnet
is a  self-cleaning, permanent, magnet
type.
  Several test  runs  were  done on the
modified system:  a standard run of 30
mm, a long-duration run of 60 min, and
surge runs from 10 to 60 sec  with
surges in feed up to 5 tph  The recovery
efficiencies varied from 95 to 98 percent.
  Samples were taken of the waste at
various points in the hammermill process.
The  samples were  analyzed for bulk
density, particle size, magnetics, and
contamination. Hammer wear and cur-
rent  and energy consumption were also
recorded.
  During the standard run, the nonmag-
netic portion in the discard tailings was
67 percent whereas the  percent con-
tamination in the magnetic product was
1.7 to 3.1 percent, well below the 4
percent criteria. In  the  long-duration
test runs on the hammermill, it appeared
that  occasional  large objects would not
cause difficulty. The specific energy was
8 98 hp/hr/ton and the power con-
sumption for the shredder was 32 hp In
the feed surge runs, only the  10-sec
runs were accomplished because the
motor current exceeded the nameplate
limit after 15 sec
  At Recovery 1, a hydraulic ram crushes
the recovered  light  ferrous product to
increase bulk density before loading
onto a railcar.  Data  from the hammer-
mill  runs  indicated that the required
density was  met, and in several cases,
compaction was unnecessary.

  To  meet the requirements for bulk
density, there had to be  a trade off in
particle size  Meeting the objective of
having only 5 percent (by weight) be less
than  1 in. proved impossible because
the magnetic concentration was typically
5 to  10 percent less  than 1 in.
  During the tuning  runs, the extent to
which the hammermill  product was
nuggetized was evaluated. An average
of 38 percent of the cans were nuggetized.
  Results of the  initial  hammermill
tuning runs and the standard run showed
an observed  hammer wear rate of 0.25
Ib/ton of magnetic concentrate passed.
The wear  rate decreased significantly,
however, during the long duration test
when 4 additional tons of ferrous con-
centrate were shredded  The overall
wear rate for the shredder using 6 tons
dropped to 0.06 Ib/ton
  Several possible improvements in the
hammermill shredder design came to
light during testing  Hard facing should
extend farther up the hammer to within
an inch of the pivot  hole  Shearing
action within the shredder might improve
if the breaker plates were modified to
contain "teeth." Additional  equipment
could be included in the design: princi-
pally, an armored belt magnet (to sepa-
rate  metal from dislodged contaminant)
and an air knife, which will  protect the
shredder from dense objects
  Results of  this test of  a shredder
followed by magnetic separation indicate
that the process effectively cleans and
densities ferrous metal without exces-
sive size reduction or nuggetizing
Product contamination is  reduced to
less than 4 percent, density is increased
to the target figure of 21.5 to 26.0 Ib/ft3
after  compaction;  and particle size
remains large enough to be used by the
detmnmg industry The shredder per-
formed satisfactorily throughout testing
although the test duration was too brief
to determine a long-term hammer wear
rate.

Test No. 4.05 and 4.09,  Air
Knife and Secondary Belt
Magnet Addition
  For these tests, the  hammermill and
the ferrous concentration system were
upgraded to  alleviate the previous
experienced deficiencies and to meet
the criteria for the high ferrous product
maximum contamination, 4 percent,
bulk density,  21.5 to  26.0  Ib/ft3;  and
shred particle size, maximum, 5 percent
less than 1  in The upgraded system
provides a ready adjustment of the drum
magnet by hydraulic activators, another
ferrous air knife, a light ferrous shredder,
and a secondary magnet. Since opera-
tion of the upgraded system began, the
new air knife adequately protected the
light ferrous shredder so that the ferrous
concentrator acts now only as a vibrating
conveyor The ferrous air  knife was
capable of handling  15,000 ftVmin of
air. The principle performance specifi-
cations were to process 5 tph of 10 to 1 5
Ib/ft3 bulk density  magnetic product
while accommodating  peak  loads of  6
tph of waste The air knife feed was to be
separated into three output streams
light  metallic  stream, light ferrous
stream, and heavy ferrous stream.
  The secondary magnet used to clean
the shredded  light ferrous is run on a  2
hp electric motor, and  a 3K-W rectifier
energizes the electromagnet. The design
air gap is approximately 7 in.
  Two processing lines, line #1 and line
#2,  feed the upgraded  system. Line #1
feeds the shredded trommel unders and
overs  ferrous  concentrate and line #2
processes scalped shredded refuse. The
estimated throughput for processing
line #2 and line #1  was 118 and 108
tph, respectively. The estimated overall
recovery for the target can ferrous metal
was 37 percent for line #1 and 48
percent for line #2.  The estimated
efficiency for  the adjustable air gap

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drum magnet was 62 percent for line #2
operation For line #1 and #2, respec-
tively, 52 percent and 64 percent of the
ferrous  metal, as cans in the air knife
feed, was recovered as product.
  In line #1 operation, 40 percent of the
target can ferrous metal (clean) was lost
to the air knife "heavies" stream; how-
ever, only 27 percent  of the lost can
ferrous  metal was "aerodynamically
light." This would bring this  loss to 12
percent if the unseparable can metal
were excluded from the feed of heavies
Line #2  operation lost 31 percent of the
can metal to the heavies; 34  percent of
which was "aerodynamically light."
This brings the loss to 12 percent.

  Of the can metal in the feed, 7 percent
was lost to the air knife "flies" or light
metallic stream in line #1 operation and
30 percent in line #2 operation. Only 1
percent of the can metal in the upgraded
system feed  was lost from the second
magnet for both lines #1 and #2 opera-
tion. About half of the contamination
attached to the can ferrous metal in the
air shredder feed was  liberated by its
processing. This reduced  the attached
contamination from 7.0 to 3.7 percent
for line #1 and from 7.9 to 4.1 percent
for line #2. The contamination of the can
ferrous  metal  in the heavies was 9.0
percent  for line #1  operation, whereas
for line #2 operation, it was 6  2 percent.
The secondary magnet of the upgraded
system carried over 9 2 and 5.4percent,
respectively, of the loose contamination
m line #1 and #2 feed. The product rate
was 1 63 tph at 26 7 Ib/ft3 and 1.34 tph
at 24 5  Ib/ft3. For both processing line
operations, the minimum required bulk
density for the product,  21 5 Ib/ft3, was
exceeded. The product  composition for
the two lines was1

               line #7, % line #2, %
loose
contamination
attached
contamination
can ferrous
noncan ferrous
ferrous less
than 1 in.
0.4
4.2
81.8
17.8
10.5
0.3
3.2
84.3
15.4
12.7
ferrous materials reporting to the lights
fraction. An increase in the blower
output with appropriate modifications of
the air  knife  interior diverters  and
baffles may be the logical next step in
improving air knife performance.
  In the ferrous stream samplings, four
sample sets were obtained under line
#2 operation and two under #1  opera-
tion  Samples were collected from the
feed,  "heavies," tailings  product, and
light nonmetallics. Data for the upgraded
process  was obtained on  volume,  bulk
density, metal weight, contamination,
and voltage and amperage used.
  During this test period, 58.1 tons of
MSW were shredded. The shredder was
run for 7 7 hr under line  #1 operating
conditions for ferrous recovery and 53 1
hr under  line  #2  conditions. For the
shredder in line #1, 24 hp were required
and the specific energy was 17 hp/hr/
ton. For line #2, 26 hp were  required
and the specific energy was 15 hp/hr/
ton The total weight loss from the
hammers during the period was 1.20 Ib,
so the wear rate was then 0.021 Ib/ton.l
It was noted that hammer wear for the
four outboard hammers was substan-
tially higher than for all  hammers.
During the 41.4 hr of line #2 operation,
one railcar was filled with 74,900 Ib of
product or a production rate of 0 90 tph.
  For the secondary  magnet, recovery
of ferrous metal was nearly 99 percent,
m spite of substantially larger-than-
design air gap

Conclusion
  Ferrous metal recovery from munici-
pal  solid waste is feasible  at a large-
scale recovery plant  However, at Re-
covery 1, the use of a trommel and
magnetic belts needed to be modified by
adding  a shredder, air knives, and
additional belt magnets.
  The full report was submitted in ful-
fillment of Contract No. 68-01-4423 by
the National  Center for Research Re-
covery, Inc., Washington, DC, under the
sponsorship  of the U S. Environmental
Protection Agency.
  The performance of the air knife met
manufacturers' design specifications
only m the case of the loose, nonme-
tallic mass split reporting to the heavy
fraction. The most serious performance
deficiency was the mass split of can
  Louis P.  Soldano is with the Municipal Environmental Research Laboratory,
    Cincinnati,  OH 45268
  Donald Oberacker and Carlton Wiles are the EPA Project Officers (see below).
  This Project Summary covers the following reports, prepared by the National
    Center for Resource Recovery, Inc,  Washington,  DC:
      "Magnetic Drum Separator Performance Scalping Trommel Underflow at
      Nominal  Design  Conditions  Test No. 401, Recovery 1, New Orleans,"
      (Order No PB 81-213 308. Cost-  $8.00,  subject to change!.
      "Magnetic  Drum Separator  Performance  Scalping Shredded  Trommel
      Overflow at Nominal Design  Conditions, Test No. 4.O3, Recovery 1, New
      Orleans.  Louisiana," (Order No PB 81-213 316. Cost  $800, subject to
      change)
      "Ferrous Metals Recovery at Recovery 1, New Orleans; Performance of the
      Modified System.  Test No  4.05 and Test  No  409, Recovery 1, New
      Orleans," (Order No PB 81 -213 324,  Cost  .$6 50. subject to  change).
      "Improvement of Magnetically  Separated Ferrous Concentrate by Shred-
      ding- A Performance Test- Test No 4.07, Recovery 1, New Orleans," (Order
      No PB 81-213 332: Cosf $8 00,  subject to change)
  All the above reports are available only from.
          National Technical Information Service
          5285 Port Royal Road
          Spring field, VA 22161
          Telephone 703-487-4650
  Donald Oberacker can be contacted at:
          Industrial Environmental Research Laboratory
          U S Environmental Protection Agency
          Cincinnati, OH 45268
  Carlton Wiles can be contacted at.
          Municipal Environmental Research Laboratory
          U S Environmental Protection Agency
          Cincinnati, OH 45268
                                                                                      •> US GOVERNMENT PRINTING OFFICE 19B1 -757-012/7264

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Environmental Protection
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Center for Environmental Research
Information
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