United States
                    Environmental Protection
                    Agency
 Municipal Environmental Research
 Laboratory
 Cincinnati OH 45268
                    Research and Development
EPA-600/S2-84-014 Mar. 1984
&ERA         Project  Summary
                    Control  of Asbestos  Fiber  Loss
                    from  Asbestos-Cement
                    Watermain
                      After the Weston, Wisconsin, Water
                     Utility discovered the deterioration of a
                     portion of its asbestos-cement water-
                     main, research to identify and effective
                     means of eliminating or reducing the
                     release  of asbestos fibers  into its
                     potable water was begun. Three tech-
                     niques were investigated: (a) using zinc
                     chloride to form a protective metallic
                     precipitate layer on the pipe surface, (b)
                     in situ cement-mortar lining of the pipe,
                     and (c) flushing of watermains. Imple-
                     mentation of the above three asbestos
                     control processes would have widely
                     differing capital and operational costs.
                      The introduction of zinc into system
                     water did  not result in the expected
                     formation  of a protective  layer  onto
                     pipe coupons, possibly because of
                     interference from polyphosphates added
                     to the system water to sequester iron
                     and manganese.  Cement-mortar lining
                     of pipe appears to be a useful technique
                     for rehabilitating still structurally sound
                     pipe. Temporary elevation of values for
                     pH  as well as calcium  and alkalinity
                     concentrations can, however, be ex-
                     pected. Flushing does not appear to be
                     an effective technique for reducing the
                     concentrations of the fibers because
                     concentration of asbestos fibers may
                     become elevated during such high draw
                     conditions. Of the three techniques
                     studied  at Weston, in situ cement
                     mortar lining was the most promising
                     approach for long term control of
                     release of asbestos fibers from deterio-
                     rating ^asbestos cement watermains.
                      This Project Summary was developed
                     by EPA's Municipal Environmental
                     Research Laboratory, Cincinnati, OH,
 to announce key findings of the research
project that is fully documented in a
separate report of the same title (see
Project Report ordering information at
back).
Introduction
  In 1980, when a Water Utility crew was
installing a tee in a 6-in. asbestos-cement
watermain, they noted that the interior of
a removed asbestos-cement pipe was very
deteriorated and that the inner wall of the
pipe was no longer as smooth as that of a
new  pipe. Because of concern for the
condition of the pipe, ways to rehabilitate
or protect asbestos-cement pipe and to
remove accumulated debris from the
mains were studied.
  This research project evaluated three
procedures for eliminating or minimizing
the number of asbestos fibers  being
released from the watermains into the
water system. The first method was to
introduce a protective zinc coating on the
pipe wall by adding zinc chloride solution
into the water supply. This procedure to
prevent the release  of asbestos  fibers
would have a low initial capital outlay but
would require perpetual annual operating
costs  associated with the necessary
chemicals.
  A second potential solution  involved
cement-mortar  lining  of the deteriorated
pipe. Although this method would require
a large  capital cost, no additional
operating and maintenance costs would
be required.
  Finally, watermain  flushing was con-
sidered as a no-cost method of potential
fiber  reduction, because flushing  is a

-------
regular operation  and  maintenance
activity.
Zinc Precipitation Treatment
  This test was designed to evaluate the
effectiveness of a precipitated zinc  pipe
coating in preventing the release of
asbestos  fibers from both new  and
deteriorated asbestos-cement pipe.  This
test subjected sample pipe coupons to the
utility's water supply treated with 1 mg/L
ZnCI2 without any adjustment of the pH of
the water and to 2  mg/L ZnCI with pH
adjustment to 8.5. Pipe sample coupons
subject to existing utility water conditions
were also included in this test as a
control.
  A  PVC pipe header was  constructed
within a lift station  located adjacent to
Fox Street. Three individual lines were
constructed; each contained a ball valve
and pressure gage for flow control and a
3/4-in.  water meter with totalizer  and
rate  of  flow  indicator.  During the  test,
flows averaged from 3.73 to 3.84 gpm. A
PVC coupon holder, constructed of 2-1/2-
in.  diameter by 6-in.  long pipe,  was
located downstream from  each water
meter. Each coupon holder was  capable
of containing two 3-in. by 1-3/4-in.  pipe
coupons held end to end. The water ca me
directly from  the distribution system,
which in turn was supplied solely from the
Mesker well.
  Pipe coupons were prepared from  both
new and  deteriorated asbestos-cement
pipe.  The pipe coupons were weighed,
without any special drying considerations,
and then placed in the coupon holders.
After the coupon test header received a
continuous flow of water for 6  mo, the
coupons were removed and weighed.
Again no particular attention was given to
the moisture content of these coupons.
When it was realized that the moisture
content of the coupons may significantly
affect the conclusions, the coupons were
shipped to the EPA research laboratory in
Cincinnati for drying and weighing. The
relative hardness of each  of the  pipe
samples was also determined  by  EPA
(Table 1).

Table 1.    Coupon Test of Zinc Treatment
  Results of hardness testing do not
show any benefits from the use of a zinc
additive at Weston. This is in contrast to
other experiments where adding zinc
helped  protect asbestos-cement  pipe.
The  lack of  positive  results for both
sample thickness measurement and
hardness testing would indicate that zinc
did not precipitate onto the pipe sample
coupons to  form a protective metallic
layer. This may have been caused by the
zinc's being  sequestered by polyphos-
phates that were added to the water to
sequester divalent iron and manganese.
Further  research  may  be  needed to
investigate the relationship between zinc
and polyphosphates.
  Coupon weight gain was inappropriate
for estimating zinc  precipitation  on
asbestos-cement pipe.  Although this
parameter may be acceptable for metallic
or plastic pipe materials,  an alternative
method of  evaluating  asbestos-cement
pipe coupons is necessary because this
pipe material  is porous  and subject to
chemical and physical reactions with
water.  For future asbestos-cement pipe
research, establishing  coupon "dry"
weight may be necessary. Because
obtaining reproducible dry weights with
this  porous  material is  difficult, and
arbitrary "dry weight" standard should
be established.  Coupon weights  were
within  1% of the 97-day dry weight after
the initial 5- to 7-day drying period, so a 5-
to 7-day drying period should be used as
such a standard.
Pipe Scraping, Polly Pigging,
and Cement Mortar Lining
  The  length of the 6-in.  asbestos-
cement watermain on which the deterior-
ation was initially discovered was sub-
divided into three tests sections labeled A
(308 ft), B (439 ft), and C (427 ft) (Figure
1). Two-inch schedule 40 PVC pipe was
constructed parallel to lines A and C to
allow recirculation of water through these
two sections. Sampling  points were
established at the one-third  and two-
     Recirculating Pump
Measurements
Avg flow, gpm
Avg zinc added, mg/L
Initial wt, gr
Wet wt after test, gr
Dry wt (5 days drying)
gr
Dry wt (97 days drying)
gr
Relative hardness.
Rockwell "L" scale
Pipe D
New Old
3.84
None
96.99
66.84
57.23

56.71

79



94.30
98.24
79.78

78.88

7

PipeE
New Old


88.82
82.45
71.12

70.38

78

3.73
1.4
97.83
90.31
72.92

72.21

-6

Pipe F
New
3.74
2.8
93.63
90.55
78.13

77.24

81

Old


77.46
89.51
72.48

71.73

5

Sternberg Ave. .



















A/C Waterrr


- T
rl

5°
Ps
^




r

•I

03
01


-[

QO
/
ai
\
/
n
r

Pi
t
1
I
1
1
1

•A/C Watermain
• 2" Recirculation
Line




r
Norma Ave.


a


• Mount View Ave.
\
i
r
ii
W
Recirculation Pump

"2" Recirculation
Line

S. T.H. "29"
figure 1.   Schematic diagram of Fox Street
           watermain test sections A, B,    1
           and C.                        *

thirds points  along the length  of each
watermain test section.
  After these sections were isolated from
the distribution system and water cus-
tomers  were  provided water from other
mains, the maintenance and rehabilitation
work began.  Pipe scraping and cement-
mortar  lining work was done under
direction  of  personnel  from Centriline
Division,  Raymond  International, Inc.
Polly pigging work was directed  by
personnel from  Becher-Hoppe Service
Corporation. Pipe samples (controls)
were taken before any work was done
and more samples were taken after
various  stages of the work. At various
times, the test sections were (1) flushed
with 700 gal of well water delivered by
tank  truck to avoid contamination  by
asbestos fibers from  the distribution
system, (2) drained, and (3) filled  with
well water, which was recirculated in the
lines for various times. The recirculated
water was sampled and analyzed for
asbestos fibers.
  Test  Section A  was  cleaned  with a
single pass of a rubber disc scraper and a
pipe sample was taken. The line was then
cleaned  with a  cable-pulled metal   ^

-------
scraper,  and another pipe sample was
taken. The line was flushed, drained, and
filled with test water. The recirculation
volume  before sampling was about
60,000 gal.
  Test Section  B, which did not have a
recirculation line and pump, was scraped
with  a metal  scraper and plugged. No
further work  was  done.  Line  C  was
flushed, drained, and filled with water for
recirculations three times after a series of
passes with different types of Polly Pigs.*
Water samples were taken after  each
series of passes; the recirculation volume
before the last sampling  was 173,700
gal. Line  C was then drained and plugged
temporarily.  Later  it was lined  with
cement mortar.
  The effects  of pipe maintenance and
rehabilitation  were evaluated in three
ways: asbestos cement pipe thickness
was  measured and the  recirculation
water was analyzed for water chemistry
changes  and for asbestos fiber content.
  Thickness of the pipe wall exceeded the
minimum wall thickness of 19.81 mm for
the Class 200 pipe used by the Town of
Weston.  Neither the scraping  nor the
pigging substantially reduced the thick-
ness of the pipe wall. Table 2 shows that
considerable variation in pipe  wall
thickness was observed.  A scanning
electron microscope showed that calcium
leaching  had occurred at the inner pipe
wall. Aggressive water  had caused
'Mention of trade names or commercial products
 does not constitute endorsement or recommendation
 for use.
calcium concentration  in the  cement
matrix of  the  asbestos-cement pipe to
decrease in depths of 2.1 to 6.5 mm into
the pipe, as measured from the inner pipe
wall-water interface (Table 2). Hardness
of the pipe specimens, both  before and
after scraping  or pigging, was less than
hardness of new pipe.
  Water quality parameters including pH,
alkalinity, and calcium  concentrations
were considerably elevated upon comple-
tion of recirculation test runs conducted
after  the  cement-mortar lining. These
elevated values are  believed to have
resulted from  the curing of the cement-
mortar material because these parameters
had  shown a  definite decreasing trend
with successive recirculation tests runs.
This sort of result would not be expected
for more than a few  days or weeks in
water distribution systems when flow is
through and out of cement-mortar lined
mains.  No flushing  action occurred
during periods of recirculation tests, and
this exaggerated the observed increases.
  When the mains wereflushed, drained,
and  filled with well  water,  which was
then  recirculated, water samples were
withdrawn for analysis. The asbestos
fiber counts (Table 3) after use of the steel
scraper and Polly Pigs  are  high when
compared with fiber  counts  in the well
water a nd the water reci rcu lated after the
cement-mortar lining  was applied. The
amphibole asbestos fibers found in  the
background water sample came from the
tank truck used to haul the well water.
  The lack of any high values (greater
than 10 million fibers per liter (MFL)) of
chrysotile asbestos fibers found after the
cement-mortar lining indicates that this
process is effective in preventing  the
release of these fibers from the deterio-
rating pipe. This is consistent with  the
96% to 99% reduction of tetrachloroethy-
lene that resulted from placing a cement-
mortar lining  over  vinyl-lined asbestos
cement pipes in a Massachusetts test.

System Flushing
  A flushing test was done in December
1981 on a  1400-ft  section of 8-in.
asbestos-cement  main (installed in
1970) on Kirk Street. This portion of the
watermain was isolated from the remain-
der of the system by closing valves as
illustrated in Figure 2. During the test,
water samples were taken  through  the
exterior hose bib at two houses on  the
street.
  This flushing test was conducted in two
distinct segments. Flow Test One con-
sisted of flushing the water in a northerly
direction along the Kirk Street watermain
and  exiting  the system at  test flow
Hydrant One.  Water for Test One was
supplied  from the nearby well and  the
250,000 gal elevated tower. In Flow Test
Two, a high velocity flow occurred in the
reverse (southerly) direction with water
supplied from the distribution system to
the west. During each test, a rate of flow
and velocity were calculated from mea-
surements of the staticand flowing water
Table 2.    Analysis of Pipe Samples Taken During Cement-Mortar Lining Evaluation
Process
Step
Background
Test line A
Control
Rubber disk scraper

Metal scraper

Test line B
Control
Metal scraper

Test line C
Control
Polyurethane pig

Red criss-cross pig
Silicon carbide pig
Wire scraper pig

Pipe Sample
New Pipe


1/3 pt. sample
2/3 pt. sample
1/3 pt. sample
2/3 pt. sample


1/3 pt. sample
2/3 pt. sample


1/3 pt. sample
2/3 pt. sample
1/3 pt. sample
2/3 pt. sample
1/3 pt. sample
2/3 pt. sample
Sample
Thickness
(mm)
21.97

21.20
21.39
20.77
21.30
20.74

21.02
21.34
21.79

21.34
22.73
21.65
25.57
22.28
22.90
20.45
Calcium*
Loss
(mm)
0.0

2.1
2.2
2.5
2.2
2.2

6.5
2.2
2.2

4.1
4.1
4.4
6.5
4.4
3.5
3.0
Mean
Ca/Si
0.83

0.57
0.80
0.6O
0.35
0.6O

0.73
0.64
0.40

0.50
0.49
0.47
0.68
0.84
0.68
0.53
Relative^
Hardness
72

2
-3
16
-11
-32

-6
-5
-8

-24
-20
-13
-15
-12
-13
-12
*'Distance measured from the interior pipe surface.
jModified Rockwell "L" hardness scale.

-------
Table3.
 Water Sample Asbestos Fiber Concentrations Taken During Cement-Mortar Lining
 Evaluation
Line
A
A
C
C
C

C

C

C

C
Process
Step
Background
After steel scraper
After first red criss cross pig
After silicon carbide coated pig
After wire pig and second red
criss cross pig
Background^

After cement-mortar lining

After cement-mortar lining

After cement-mortar lining.
Asbestos
Amphibole (MFL)*
0.32
ND
ND
o.ret
0.37t
ND
ND
ND
ND
ND
ND
ND
ND
Fibers
Chrysolite {MFL)
1.6
8.4
87.5
10.9
8.4
49.2
ND
1.71
0.35f
2.1
ND
1.6
1.3
             line drained, flushed, and filled
             a second time
C

C


Background^

After cement-mortar lining.
line drained, flushed, and
filled a third time
ND
ND
ND
ND

0.131:
0.42\
0.44\
ND

*MFL - Million fibers per liter.
t/Vof statistically significant, less than 5 fibers counted.
^Municipal well water samples from the tank truck.
§Mesker Street well hydrant sample.
Note: Two values are reported where replicate samples were analyzed.
                                                                       not result in protection of asbestos-
                                                                       cement pipe.
                                                                    •  Disturbing the inner wall of asbestos-
                                                                       cement pipe by scraping or  by using
                                                                       Polly Pigs resulted in high asbestos
                                                                       fiber  counts in water  that passed
                                                                       through the treated pipes.
                                                                    •  Lining asbestos-cement  pipes with
                                                                       cement mortar is feasible.  Cement
                                                                       mortar lining can be applied to
                                                                       asbestos-cement pipes.
                                                                    •  Eliminating or substantially reducing
                                                                       the asbestos-fiber contamination of
                                                                       potable water from asbestos-cement
                                                                       pipes is  possible with the  cement
                                                                       linning procedure.
                                                                     The full report was  submitted in
                                                                   fulfillment of Cooperative Agreement CR-
                                                                   808476010  by Weston  Water Utility,
                                                                   Schofield, Wl  54476 under the sponsor-
                                                                   ship of the U.S. Environmental Protection
                                                                   Agency.
           \   • Valves Closed Both Tests
 Test 2 Water
   Supply
  I Closed Test 1
  i Open Test 2  \
6102 Kirk St. XT
Sample Point  g
Test 1 &2    $>
             •£
             £

                Test 1 Flow Hyd.
AC. Flow
Test Main


6303 Kirk St.
Sample Point Test 2
Open Test 1
Closed Test 2
   .J_
                          250,000 Gal.
                          EL. Tower
                                flushing test and the chrysotile asbestos
                                fiber concentrations are given in Table 4.
                                  The flushing test revealed that chryso-
                                tile fiber counts were somewhat elevated
                                when compared with  counts for undis-
                                turbed  water,  even  after  90 min of
                                flushing. Other studies have indicated
                                that  main  flushing results in higher
                                asbestos fiber counts, possibly by stirring
                                up asbestos-laden sediment in the mains.
                                Further testing  is needed before recom-
                                mendations  concerning flushing of
                                asbestos-cement  watermains can be
                                made.

                                Conclusions
                                  •  Using zinc as a corrosion inhibitor in
                                    the presence of polyphosphates may
                        ——"	^—,    Table. 4.    Flushing Tests and Chrysotile Asbestos Fiber Concentrations
Test 2 Flow Hyd. From Well I
I
Test 1 Water
Supply
2. Schematic diagram of flushing
test on Kirk Street.
Sample
Station
Test No. 1
Background
6102 Kirk Street
6102 Kirk Street
6102 Kirk Street
Test Condition
Flushing, 25 min
Waiting period, additional 85 min
Waiting period, additional 90 min
Chrysotile
Concentration,
MFL*
0. 18 MFL, NSS*
3.22 MFL
9.95 MFL
76. 1 MFL
Figure 2.
pressures recorded at the  discharge
hydrant. The flow during Test One was
approximately  1,100 gpm with  an  ap-
proximate velocity of 7 ft/s. During Test
Two, the flow was calculated to be 820
gpm  with an average velocity of 5 ft/s.
The  procedures followed during  the
                                          Test No. 2 (Valves at Test Hydrant 2 opened and closed (Figure 2)
                                 6102 Kirk Street Sample
                                 6303 Kirk Street
                                 6102 Kirk Street
                                               Waiting period, 15 min
                                               Waiting period, additional 25 min
                                               Hydrants closed and all valves
                                               opened; waiting period, 6 days
No fibers detected
7.32 MFL
0.15 MFL. NS
                                 'Million fibers per liter.
                                 *Not statistically significant

-------
     This Project Summary was prepared'by staffofthe Town of Weston, Schofield. Wl
      54476.
     Gary S. Logsdon is the EPA Project Officer (see below).
     The complete report, entitled "Control of Asbestos Fiber Loss from Asbestos-
      Cement Watermain," (Order No. PB 84-148 733; Cost:  $10.00. subject to
      change) will be available only from:
            National Technical Information Service
            5285 Port Royal Road
            Springfield, VA 22161
             Telephone: 703-487-4650
     The EPA Project Officer can be contacted at:
            Municipal Environmental Research Laboratory
            U.S.  Environmental Protection Agency
            Cincinnati, OH 45268
United States
Environmental Protection
Agency
Center for Environmental Research
Information
Cincinnati OH 45268
..--^J.3. OFr SCiAL '/'Ali.
  ' "             ~'
                                                                                         ("Adie-3--.
Official Business
Penalty for Private Use $300
                                                                                   U.S. GOVERNMENT PRINTING OFFICE: 1984-759-
                                                                                                                    102/089^

-------