United States
                   Environmental Protection
                   Agency
Robert S. Kerr Environmental
Research Laboratory
Ada OK 74820
                   Research and Development
EPA-600/S2-84-176 Jan. 1985
&ERA         Project Summary
                   Demonstration  of  a  Maximum
                   Recycle,  Sidestream  Softening
                   System  at a  Petrochemical
                   Plant  and a  Petroleum  Refinery
                   Jack V. Matson, Wendy Gardiner Mouche, Eric Rosenblum, and
                   Larry McGaughey
                    New full-scale  maximum  recycle
                   sidestream softening systems at USS
                   Chemicals, Houston, Texas, and TOSCO
                   Refinery, Bakersfield. California, were
                   evaluated as a technology to achieve
                   zero wastewater discharge.  Softener
                   process efficiency was optimum at a pH
                   control range of 10.3 to 10.5 at 40°C
                   and using a high mixing intensity. A
                   problem of heat exchanger biofouling
                   from the high dissolved organics in
                   recycle water was effectively controlled
                   by using  Bromocide with chlorine. A
                   total organic carbon balance over the
                   cooling  water system showed raw
                   makeup water and process water con-
                   tribute 1 /3 and 2/3 of the organics,
                   respectively. Major organic sinks were
                   drift (60%), biodegradation (30%), and
                   volatilization (10%). Softener sludge as
                   analyzed for chromium by leachate tests
                   was classified  as nontoxic. Heat ex-
                   changer  equipment  averaged two
                   mils/year internal corrosion.  External
                   corrosion from drift aerosols was cor-
                   rected by installation of a ferrous sulfate
                   reactor in the blow down system and
                   improved drift eliminators in  cooling
                   towers. The TOSCO water problem of
                   high silica and low magnesium was
                   corrected by adding caustic and mag-
                   nesium sulfate to the softener. Both
                   plants operated satisfactorily  at near
                   zero liquid discharge. Operating costs
                   and benefits are discussed.
                    This Project Summary was developed
                   by EPA's Robert S. Kerr Environmental
                   Research Laboratory, Ada. OK, to an-
nounce key findings of the research
project that is fully documented in a
separate report of the same title (see
Project Report ordering information at
back).

Introduction
  The USS Chemicals plant in Houston
produces ethylene from a refinery gas
rich in ethane by a steam cracking
process, and manufactures styrene from
ethyl-benzene by a catalytic process. The
plant is medium sized, with 200 em-
ployees.
  Prior to  1979, the plant discharged
roughly 300 to 500 gallons per minute of
effluent to the Houston Ship Channel.
The wastewaters consisted primarily of
oily condensates from the ethylene unit
that were  collected  and treated in a
coagulation/flocculation unit and added
to the cooling water systems. The blow-
down from these systems with plant
runoff and demineralizer spent regenera-
tion fluid constituted the effluent.
  The regulations governing the quality
of the effluent were made more stringent
in a stepwise fashion starting in 1974. At
that time, USS Chemicals initiated a water
management study to determine the need
for wastewater treatment facilities. Var-
ious schemes for upgrading the existing
facilities such as biological treatment,
dirty boiler, and activated carbon were
compared to the sidestream softening
recycle system. The study showed that
the waste from other systems was not
very biodegradable or adsorbable. On the

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basis of economics, the recycle system
was chosen.  The  savings  in  water
makeup, which was from a surface water
delivery system, coupled with the reality
that there were  no  feasible alternative
treatment processes, resulted in a deci-
sion to choose the current system.
  The strategy for successful implemen-
tation would be quite simple. The chemi-
cal  scale from  constituents—calcium,
magnesium, and silica—would  be  re-
moved in the softener. The other ions,
such as  sodium,  chloride, and sulfate,
would be concentrated and controlled by
drift, the  aerosol droplets escaping with
the heated air from the cooling tower. The
potential  problems were high total dis-
solved  solids (TDS), which increased the
corrosivity of the cooling water; concen-
tration of non-volatile  organics,  which
increased the biofouling  potential; and
external corrosion from the deposition of
the drift aerosols.
  The potential advantages were elimi-
nation  of blowdown, which was  the
largest quantitative source of effluent
requiring treatment prior to discharge;
savings in makeup water; and a way to
continue to  use chromate corrosion in-
hibitors. Hexavalent chrome was found to
be  toxic  at  low  concentrations  so that
regulations  called for nearly complete
removal.  At that time,  there were no
equivalent substitutes for chromate as a
corrosion inhibitor.
  Pilot testwork of the proposed system
was conducted in 1974-75. Construction
began  in 1977 and coincided with  the
conversion from ground water to surface
water supply. The entire facility, including
surface water treatment  units,  had a
capital cost of roughly $3 million of which
half the  cost  was  for the sidestream
softening system.
  This system was unique in a  number of
ways.  First, carbon  dioxide instead of
sulf uric acid was used to control pH in the
cooling water system. The reasoning was
that carbon  dioxide preserved the bicar-
bonate in the raw water, and thus greatly
reduced  the need for soda ash m  the
sidestream softeners. Sulfuric acid would
have destroyed the  bicarbonate by con-
verting it to carbon dioxide  that was
strippable in the cooling towers. Another
important reason for carbon dioxide usage
was that  the pH in the cooling water could
only go as low as approximately four in
the event of operator error or equipment
malfunction, while sulf uric acid overdose
could bring the pH significantly lower and
damage the heat exchangers, which were
of  carbon  steel  with  some stainless
material.
  All process water was collected, treated
(if necessary), and used as makeup to the
cooling water system. This included oily
condensates which were treated in an
API separator and  a coagulation/floc-
culation process, boiler  blowdown, and
plant  runoff including storm water. The
only discharge was the high  TDS de-
mineralizer-regeneration water. Prior to
this project, the effluent discharge was in
the range of 300 to 500 GPM; afterwards,
it was 30 to 50 GPM, a ten-fold reduction.


Study Objective
  The objectives of the  study  were as
follows:

  1.  evaluate the performance of the
     sidestream softening system;
  2.  determine the impact of the recycle
     streams on the  cooling water
     system;
  3.  discover  the fate  of  the  organic
     matter in the cooling water system;
     and
  4.  investigate  the potential sludge'
     disposal problems.

Findings

/.  Performance Evaluation
  Prior to startup, there were two impor-
tant questions. First, was there sufficient
magnesium  in the raw water to adsorb
the silica in the softening reactions? The
silica-to-magnesium ratio  in  the  raw
water was two to one (in mg/L), which
was marginal. In the reaction, magnesium
is precipitated as a hydroxide onto which
the silica is adsorbed. The question was
answered in the affirmative. As part  of
the project, a detailed scientific delinea-
tion of the adsorption phenomena  was
made.
  The  second  question involved the
selection of the appropriate scale inhibitor
for the cooling water. An inhibitor was
needed that worked well in the cooling
water but did not significantly  interfere
with the  softening reactions.   Generic
phosphonate inhibitors  were found  in
laboratory tests to work  too well in that
the efficiency of the softening reactions
was decreased. Selected were polymaleic
anhydride polymers which  mechanisti-
cally prevented scale formation by fluidiz-
ing small crystals rather than inhibiting
crystal formation. That is what  actually
happened. The inhibitor helped  maintain
a scale-free  heat transfer system.
  The most  critical element of the side-
stream softening system was the soften-
 ers. Operational costs were related to the
 consumption of soda ash and lime in the
 softening process as was process  effi-
 ciency. So it was important to develop the
 optimum control strategy for the system.
   The lime dosage controlled the pH  of
 the reaction in the  softener.  Soda ash
 was used to make up for any deficiency in
 carbonate in the reactor. With the use of
 carbon  dioxide  in  the cooling  water
 system, the bicarbonate in the makeup
 water was conserved so that the soda ash
 requirement was minimized. The opera-
 tors were instructed to control pH within
 a narrow band by lime addition,  and  to
 add soda ash based on the  difference
5 between the calcium hardness  and
 carbonate alkalinity run every four hours.
   The objective of this part of the per-
 formance evaluation was to define the
 most cost-effective pH in the softeners
 with quality constraints  in the cooling
 water. The interactions were as follows.
 A higher  pH  required  a greater  lime
 dosage and increased the soda ash usage
 as  more carbonate  was  necessary  to
 react with the calcium ions in the lime.
 However, the higher pH improved reaction
 efficiency by  conversion  of  a  greater
 percentage of bicarbonate to carbonate
 and precipitation of magnesium. Thus, for
 a greater cost, the benefit was a higher
 reaction efficiency, which allowed for a
 decreased flow requirement through the
 softeners. The optimization studies per-
 formed in the laboratory then in the plant
 indicated that the control pH  range was
 10.3 to 10.5 at40°C.
   The next performance problem analyzed
 was the effect of mixing intensity on the
 softening reactions. The softeners were
 manufactured by Infilco Degrement under
 the Densator brand name. Of particular
 interest was  the  mixing in the primary
 reaction zone.
   Originally, a blade arm rotating on the
 same shaft as the bottom scraper provided
 slow speed mixing.  It appeared to  be
 inadequate; so two high-speed turbine
 mixers replaced the blade in one softener
 while the other softener retained the
 blade for comparison purposes.
   The results of the testing indicated that
 mixing intensity was, indeed, an impor-
 tant variable. At low mixing intensities,
 the reaction/adsorption process involving
 magnesium precipitating as the oxide and
 the subsequent adsorption of silica was
 adversely affected. Also the lime dosage
 was much greater because its dissolution
 was strongly  influenced by mixing.  At
 very high mixing intensities, the clarifica-
 tion process was hindered by the breakup
 of the particles. Thus, an optimum mixing

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intensity with the  turbine mixers was
defined.
  Two other observations are worth
noting: with the slow-speed blade it was
difficult to control the addition of lime and
soda ash to the softeners because the
reaction zone was not well mixed, which
created sampling errors, inaccurate test
results, and high feedback control noise.
Also, silica  adsorption in the reactor was
much higher than previously predicted in
laboratory studies.

2.  Impact of Recycled Water
  The  recycle water that had a strong
negative  impact on the  cooling water
system was  the process wastewater
which  was high in dissolved  organics.
After the startup and shakedown of the
sidestream  softening system, the major
unresolved  problem was biofouling in the
heat exchange system. It was particularly
bad on the critical  surface condensers.
The problem was  exacerbated  by  the
operation conditions in the cooling water
system. As previously mentioned, carbon
dioxide was used to maintain pH control.
To minimize the use and expense of the
gas, which was readily stripped out in the
cooling tower, the  pH  was maintained
between 7.6 and 7.8. Chlorine was used
as the primary biofouling control agent.
At the  higher pH, chlorine was relatively
ineffective, as it  was  largely  in  the
hypochlorite ion state. Thus, a research
effort  was  undertaken to resolve  the
problem. An organic compound, dichloro-
dibromo dydantoin  (trade name  Bromo-
cide)  was  added  in conjunction  with
chlorine. The combination of these chem-
icals  proved to be  very effective in
controlling biofilm development  at a
reasonable cost. The key was bromine
which, when released in solution  as
hypobromous acid,  was an effective bio-
cide at the higher pH.

3.  The Fate of  Organics
  A total organic  carbon  balance was
made over  the cooling  water system to
determine the sources  and sinks of the
organic material. Samples were analyzed
for biodegradability. The results indicated
that the raw makeup water and  the
process water contribute one-third  and
two-thirds of the organic materials,
respectively. The major sinks were drift
(60%), biodegradation (30%), and volatil-
ization (10%).

4.  Sludge Disposal
  The  most  serious  potential problem
with the sludge from the softeners was
the classification,  i.e., whether it  was
considered toxic and had to be disposed of
in a Class 1 site at high cost. The  only
constituent  of concern  was chromium
used  in the cooling water system  as a
corrosion inhibitor. A fraction  of it de-
graded  from a  hexavalent form  to a
trivalent form  that  precipitated  as a
hydroxide in the softeners.
  A series of  leachate tests were  per-
formed using both the EPA Standard and
State of Texas procedures. Under a variety
of conditions at the plant and in the lab,
the sludge met both the  EPA and State
criteria.  The sludge was consequently
classified as non-toxic.

Other Investigations
  After startup, the cooling water system
equilibrated  at a total dissolved solids
(TDS) level between 20 and 30,000 mg/L.
This figure was much higher than origi-
nally anticipated. Internal corrosion in the
heat exchange equipment was never a
problem, averaging below two  mils per
year during the course  of the study.
However, external  corrosion caused by
the deposition  of drift aerosols by  sur-
rounding equipment was a real concern.
As  part  of  the  study,  an  emergency
blowdown system consisting of a reactor
in which ferrous sulfate  was  added to
precipitate the chromate  and a clarifier
was tested in the laboratory. As a result of
the tests, a full-scale treatment system
was placed into operation. Also, the major
cooling tower was rebuilt with improved
drift eliminators to  minimize the deposi-
tion.

Summary—USS Chemicals
  The sidestream softening concept  was
particularly attractive to USS Chemicals
because the cost  of their  water  was
relatively high and their effluent  dis-
charge  regulations  were tough.  The
system  is continuing to operate   in a
steady-state mode, achieving the original
expectation with a minimum discharge.

TOSCO
  At TOSCO, different reasons existed for
considering  zero discharge, sidestream
softening. In the past the effluent  had
been  discharged into a percolation  field
from  which it  migrated into an under-
ground aquifer. As regulations stiffened,
the discharges were shifted to an injection
well system at the refinery. The injection
well was costly to operate, and was taxed
by the State as a hazardous waste.
  Since the cooling water blowdown was
a  major volumetric constituent in the
injection well, it made economic sense to
look for alternative ways to deal with it. In
the mid-1970's several studies favorably
evaluated sidestream softening for the
blowdown. In  1980, the decision to
proceed with that design was made.
  The unique problem with the TOSCO
water was its  high silica and low mag-
nesium content. Insufficient magnesium
was present in the makeup water to have
much adsorbing power for the silica. An
evaluation of alternative ways to over-
come the problem indicated that the best
way was a combination  of caustic as the
source of hydroxide in the softener and
magnesium  sulfate as the  source of
soluble magnesium for silica reduction.
  Laboratory  studies had shown that
magnesium in a soluble form had roughly
an order of magnitude greater adsorbing
power for silica than solid forms such as
magnesium  oxide  and  dolomitic lime.
Caustic was attractive as a way to mini-
mize sludge production and soda ash
usage.
  The system consisted  of dual Densator
softeners, sulfuric acid  pH control tank,
and dual media filters.  The sludge was
concentrated and pumped to a  series of
lined evaporation ponds.
  The refinery consisted of five cooling
water systems with a combined recircula-
tion rate of 53,000 gpm,  tied together.
Design  flow  through  the  sidestream
softener was rated for 250 gpm, of which
150 was from the cooling water system,
and the remainder from the boiler blow-
down and scrubber system.

Operation and Economics
  Startup commenced smoothly in March
1982, with the system running at steady
state within  one week.  A dense sludge
was quickly established  in the softeners.
Silica was controlled to below 150 mg/L
in the cooling water  system  by the
measured addition of dissolved magne-
sium. The total dissolved solids level
fluctuated between  5,000 and  8,000
mg/L.
  Reuse  of cooling water saved TOSCO
roughly  $36,000 in actual water costs.
Another  $300,000 was saved in supply
well maintenance,  power, and taxes.
Water  treatment  chemical  savings of
$50,000  were also realized.  Overall,
savings for the refinery were estimated at
$500,000 per year. The cost of the side-
stream softening system was $2.5 mil-
lion. The  capital payback period is five
years.

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     J.  V. Matson,  W. G. Mouche, E. Rosenblum, and L McGaughey are with the
       University of Houston, Houston, TX 77004.
     Donald Kampbell is the EPA Project Officer (see below).
     The complete report, entitled "Demonstration of a Maximum Recycle, Sidestream
       Softening System at a Petrochemical Plant and a Petroleum Refinery," (Order
       No. PB85-121 044; Cost: $19.00, subject to change) will be available only from:
             National Technical Information Service
             5285  Port Royal Road
             Springfield, VA 22161
             Telephone: 703-487-4650
     The EPA Project Officer can be contacted at:
             Robert S. Kerr Environmental Research Laboratory
             U.S. Environmental Protection Agency
             P.O. Box 1198
             Ada. OK 74820
   * U.S GOVERNMENT PRINTING OFFICE; 1985 — 559-016/7885
United States
Environmental Protection
Agency
Center for Environmental Research
Information
Cincinnati OH 45268
".'•:  .    '"  PDSTA4l«rJpEE&«AiO
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                                                                                                          PERMIT No. G-35  *
Official Business
Penalty for Private Use $300

                        1L  60604

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