United States
                    Environmental Protection
                    Agency
Air and Energy Engineering
Research Laboratory
Research Triangle Park NC 27711
                    Research and Development
EPA/600/S2-86/068 Nov. 1986
oEPA          Project Summary

                    Microprocessor  Control  of
                    Rotogravure  Airflows
                    D. R. Rosen and M. R. Wool
                     This report discusses the technical
                    and economic viability of using
                    microprocessor-based control technol-
                    ogy to collect volatile organic com-
                    pound (VOC) emissions from a paper
                    coating operation. The system evalu-
                    ated is operating at the James River
                    Corporation rotogravure printing facil-
                    ity in Kalamazoo, Michigan.
                     The microprocessor-based control
                    system monitors and controls both the
                    airflow rate and vapor concentration
                    level within the printing press dryers. It
                    enables incineration of the VOC emis-
                    sions in the plant's existing steam
                    boiler and also saves energy by reduc-
                    ing the amount of dryer and room air
                    that must be heated. The general con-
                    cept, performance levels, and economic
                    parameters for the James River VOC
                    control system demonstrate the poten-
                    tial advantages of the technology for a
                    wide range of applications.
                     James River looked at three methods
                    to collect and destroy VOC emissions
                    for their rotogravure operation: solvent
                    recovery, thermal destruction in a dedi-
                    cated incinerator, and thermal destruc-
                    tion in an existing onsite boiler. For
                    James River, the use of their existing
                    boiler is the best option even though
                    they were required to add equipment to
                    collect, transport, and control the ro-
                    togravure airflows.
                     The microprocessor and sensors
                    which are an integral part of the emis-
                    sion control system enable James River
                    to safely reduce the flowrate of air
                    through their  presses. The sensors
                    measure the air pressure and VOC con-
                    centration in the press dryer exhaust,
                    and the microprocessor adjusts fan
                    speeds to maintain proper flowrates.
                     Over a 3-day period, operating data
                    were recorded to evaluate the flow sys-
tems performance. With the microproc-
essor in operation, James River ex-
pected to see flowrates of less than
30% of the flow prior to conversion.
This expectation was confirmed  by
measurements taken  during the test
period. Despite the flowrate reduction,
concentrations of VOCs remained
safely below the lower flammability
limit. These tests showed that a micro-
processor system, appropriately tied to
an incinerator or boiler, is an effective
way to address federal and state VOC
emission standards for the paper print-
ing industry.
  This Project Summary was devel-
oped by EPA's Air and Energy Engineer-
ing Research Laboratory, Research Tri-
angle Park,  NC, to  announce key
findings of the research project that is
fully documented in a separate report
of the same title (see Project Report or-
dering information at back).

Introduction
  The microprocessor-based control
system monitors and controls both the
airflow rate and vapor concentration
level within the printing press dryers.
The system in  this study incinerates
VOC emissions in the plant's existing
steam boiler and also saves energy by
reducing the amount of dryer and room
air that must be heated. The general
concept, performance levels, and eco-
nomic parameters for the VOC control
strategy demonstrated the potential ad-
vantages of  microprocessor control
technology for a wide  range of applica-
tions.
  This study discusses the technical
and economic viability  of using
microprocessor-based control technol-
ogy to  collect volatile organic  com-
pound (VOC)  emissions from  a paper

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c6ating  operation. The system evalu-
atecj^s operating at the James River
Corporation rotogravure printing facil-
ity^ n Kalamazoo, Michigan.

System Installation Objective
  VOC emissions react in the atmos-
phere to form ozone and other undesir-
able constituents of smog. As a result,
James River Corporation initiated a pro-
gram  to control atmospheric emission
of VOCs from their rotogravure printing
operation. The  objective of installing
the control system was to collect and
destroy VOC  emissions by the most
cost-effective approach.

System Elements
  A microprocessor-based system was
selected by the James River Corpora-
tion to safely  lower dryer airflows and
permit VOC incineration in an existing
process boiler. The microprocessor sys-
tem automatically controls exhaust fan
speeds to minimize airflow rates while
maintaining safe  VOC concentrations.
The net reduction in  flow  allows the
existing process boiler to accept all ro-
togravure dryer emissions as combus-
tion air.
  The major elements of the VOC con-
trol and collection system at the James
River  plant are:
  • A microprocessor based computer/
    controller.
  • A continuous analyzer to determine
    when VOC concentrations  ap-
    proach the lower flammability limit
    (LFL).
  • Variable speed motor drives.
  • Pressure transducers.
  • Diversion dampers.
  • Operator display panel.
  Several other modifications and sub-
systems were also necessary to imple-
ment  VOC destruction using the exist-
ing plant boiler. Ductwork was installed
between a transfer fan and the boiler
forced draft fan. A new forced draft fan
was installed because the existing fan's
bearings  would  be damaged by the
VOCs in the press exhaust aiu Modifica-
tions were also necessary to some press
decks in order to provide better sealing,
thereby allowing  operation  at reduced
fan speeds.

Performance Data  Acquisition
  As a part of the VOC control system,
process parameters are monitored by
permanent instrumentation. However,
the existing system has no provisions
for data storage. Therefore, process
parameters of  interest to  this study
were recorded during the test period by
a temporary  data acquisition  system.
The system consisted of a data interface
unit and a personal computer. A floppy
disk and thermal  printer provided for
hardcopy data output and storage.

Performance Results
  Table 1 shows the effect of the VOC
control system  on the flowrate  of  air
through the four presses considered in
this study and confirms that the system
operated as  expected during the data
acquisition period.  Measured airflow
rates were close to the expected values,
which represented a 71%  decrease in
airflow when compared to  the precon-
version values. Despite the decrease in
airflow rates, the percentage LFL re-
mained well within acceptable and safe
values.

Equipment Cost and Energy
Savings
  This installation of a microprocessor
control system enables the plant's exist-
ing boiler to be used for VOC  destruc-
tion. James River determined that use
of the existing boiler was the most cost-
effective method  of addressing their
VOC emission control requirements. In
addition, significant cost savings result
from operation  of the system  because
the quantity of collected air was signifi-
cantly reduced. These savings include:
  • Reduction in  energy demand for
    dryer air heating due to reduced air
    exhaust rates.
  • Recovery of thermal energy in
    press exhaust by using the exhaust
    as air for boiler combustion (presi
    exhaust averages 23°C above ambi
    ent air temperatures annually).
  • Recovery of calorific value of VOCs
    incinerated in the boiler.
  Table  2 summarizes installed cost
for the conversion project at the Jame!
River plant. Annual energy savings an
summarized in Table 3.

Safety
  The control system incorporates sev
eral  safety features and interlocks,  in
eluding:
  • LFL analyzer failure (flameout) de
    tection.
  • High LFL level alarm  and pres:
    shutdown.
  • Loss of deck exhaust flow.
No LFL analyzer  failures occurred dur
ing the data collection period, nor wen
acceptable  percentage LFL levels ex
ceeded.  Based on the review of the sys
tern design and  operating data, thesi
safety features operated as intended.


Conclusions
  This study shows that rotogravur
printing operations can benefit from th
microprocessor-based control techno
ogy discussed in this report. Economi
benefit accrues due to the reduction i
process air exhaust  volumes whic
must be processed by a collection syi
tern or  an  incinerator  or heated by
process dryer. The techniques used t
monitor and control  VOC  concentn
tions and to allow lower air volumes at
broadly applicable to  processes whic
Table 1.    VOC Collection System Performance Summary
                                                After conversion
Press
No.
3047
3049
3051
3052
rnor to conversion
Exhaust flowrate
scfm
(l/s)
20,000
(9,378)
25,000
(11.723)
7,000
(3,282)
25,000
(11,723)
77,000
(36,106)'
Expected exhaust
flowrate
scfm
(l/s)
6,000
(2,813)
4,000
(1,876)
4,200
(1,969)
8,000
(3,751)
22,200
(10,409)"
Measured exhaut
flowrate
scfm
(l/s)
6,105
(2,863)
3,839
(1,800)
4,245
(1,990)
7,900
(3,704)
22,089
(10,357)a
"Totals have been rounded off for consistency.

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 Table 2.    Conversion Cost Summary—1985 Dollars

                Category
                                Total
                              ($1000s)
 Control System
 1. Microprocessor control system3
 2. LFL Analyzers"
   Subtotal
 Engineering
 3. Preinstallation analysis and system design
 Collection and Transport System0
 t. Ducting and press modifications
 5. Boiler modifications
   Subtotal
   Total
                                 295
                                 145
                                 440

                                 100

                                 720
                                 300
                                1020
                                1560
 'Includes computer, pressure transducers, and drives.
 'Includes two FID analyzers, eight-channel manifold, and sample pump.
 '•Items 4 and 5 are unique costs, required only because James River was ducting to a boiler. If
 the plant had an existing incinerator, then these costs would not be applicable.
"able 3. Annual Fuel Energy Savings
Air reduction
Units savings
3tu x Jfl6 34,250
loules x JO9 36,727
Air preheat
savings
12,670
13,364
Calorific
value
24,930
26,296
Total
71,850
75,787
 use heated air in the presence of sol-
 vents or other materials. The system re-
 duces plant operating and  pollution
 control costs by reducing fuel required
 to heat the facility air or the air used in
 the process.
  The application of microprocessor
 technology studied at James River is an
 extension of the technology from metal
 coating (i.e., painting) application. This
 study proved that the technology is ap-
 plicable to the paper coating industry
 and can provide  economic  benefits
 through the reduction in energy  re-
 quirements for a  printing process.  Al-
 though the amount of energy savings
 and the cost of plant modifications will
 be different for each application, energy
 savings, in most cases should offset the
 capital  cost of the plant modifications
 within a short time. Additional reduc-
 tions in operating costs will also be real-
 ized due to the reduced airflows.
  A potential user of a microprocessor
control  system should review the re-
sults of this study  to assess  if similar
energy  and emission control  benefits
are possible in other applications of in-
terest. In general, any application where
airflows are used to carry away VOCs
could be improved through active con-
trol of both airflow rates and VOC con-
centrations. Depending on the applica-
tion, the b*st cleanup approach may be:
  • Corr4in'stion in a dedicated inciner-
    ator.
  • Combustion  in  an available plant
    boiler.
  • Collection in a VOC recovery facil-
    ity.
The best choice in a given situation will
depend on the VOC quantities, airflow
rates, plant layout,  other plant equip-
ment, energy costs, and permitting re-
quirements.

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        D. Rosen andM. Wool are withAcurex Corporation. Mountain View, CA 94039.
        Charles H. Darvin is the EPA Project Officer (see below).
        The complete report, entitled "Microprocessor Control of Rotogravure Airflows."
         (Order No. PB 86-230 075/AS; Cost:  $11.95. subject to change) will be
         available only from:
                National Technical Information Service
                5285 Port Royal Road
                Springfield. VA 22161
                Telephone: 703-487-4650
        The EPA Project Officer can be contacted at:
                Air and Energy Engineering Research Laboratory
                U.S. Environmental Protection Agency
                Research Triangle Park. NC 27711
United States
Environmental Protection
Agency
Center for Environmental Research
Information
Cincinnati OH 45268
Official Business
Penalty for Private Use $300
EPA/600/S2-86/068

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