United States Environmental Protection Agency Air and Energy Engineering Research Laboratory Research Triangle Park NC 27711 Research and Development EPA/600/S2-86/068 Nov. 1986 oEPA Project Summary Microprocessor Control of Rotogravure Airflows D. R. Rosen and M. R. Wool This report discusses the technical and economic viability of using microprocessor-based control technol- ogy to collect volatile organic com- pound (VOC) emissions from a paper coating operation. The system evalu- ated is operating at the James River Corporation rotogravure printing facil- ity in Kalamazoo, Michigan. The microprocessor-based control system monitors and controls both the airflow rate and vapor concentration level within the printing press dryers. It enables incineration of the VOC emis- sions in the plant's existing steam boiler and also saves energy by reduc- ing the amount of dryer and room air that must be heated. The general con- cept, performance levels, and economic parameters for the James River VOC control system demonstrate the poten- tial advantages of the technology for a wide range of applications. James River looked at three methods to collect and destroy VOC emissions for their rotogravure operation: solvent recovery, thermal destruction in a dedi- cated incinerator, and thermal destruc- tion in an existing onsite boiler. For James River, the use of their existing boiler is the best option even though they were required to add equipment to collect, transport, and control the ro- togravure airflows. The microprocessor and sensors which are an integral part of the emis- sion control system enable James River to safely reduce the flowrate of air through their presses. The sensors measure the air pressure and VOC con- centration in the press dryer exhaust, and the microprocessor adjusts fan speeds to maintain proper flowrates. Over a 3-day period, operating data were recorded to evaluate the flow sys- tems performance. With the microproc- essor in operation, James River ex- pected to see flowrates of less than 30% of the flow prior to conversion. This expectation was confirmed by measurements taken during the test period. Despite the flowrate reduction, concentrations of VOCs remained safely below the lower flammability limit. These tests showed that a micro- processor system, appropriately tied to an incinerator or boiler, is an effective way to address federal and state VOC emission standards for the paper print- ing industry. This Project Summary was devel- oped by EPA's Air and Energy Engineer- ing Research Laboratory, Research Tri- angle Park, NC, to announce key findings of the research project that is fully documented in a separate report of the same title (see Project Report or- dering information at back). Introduction The microprocessor-based control system monitors and controls both the airflow rate and vapor concentration level within the printing press dryers. The system in this study incinerates VOC emissions in the plant's existing steam boiler and also saves energy by reducing the amount of dryer and room air that must be heated. The general concept, performance levels, and eco- nomic parameters for the VOC control strategy demonstrated the potential ad- vantages of microprocessor control technology for a wide range of applica- tions. This study discusses the technical and economic viability of using microprocessor-based control technol- ogy to collect volatile organic com- pound (VOC) emissions from a paper ------- c6ating operation. The system evalu- atecj^s operating at the James River Corporation rotogravure printing facil- ity^ n Kalamazoo, Michigan. System Installation Objective VOC emissions react in the atmos- phere to form ozone and other undesir- able constituents of smog. As a result, James River Corporation initiated a pro- gram to control atmospheric emission of VOCs from their rotogravure printing operation. The objective of installing the control system was to collect and destroy VOC emissions by the most cost-effective approach. System Elements A microprocessor-based system was selected by the James River Corpora- tion to safely lower dryer airflows and permit VOC incineration in an existing process boiler. The microprocessor sys- tem automatically controls exhaust fan speeds to minimize airflow rates while maintaining safe VOC concentrations. The net reduction in flow allows the existing process boiler to accept all ro- togravure dryer emissions as combus- tion air. The major elements of the VOC con- trol and collection system at the James River plant are: A microprocessor based computer/ controller. A continuous analyzer to determine when VOC concentrations ap- proach the lower flammability limit (LFL). Variable speed motor drives. Pressure transducers. Diversion dampers. Operator display panel. Several other modifications and sub- systems were also necessary to imple- ment VOC destruction using the exist- ing plant boiler. Ductwork was installed between a transfer fan and the boiler forced draft fan. A new forced draft fan was installed because the existing fan's bearings would be damaged by the VOCs in the press exhaust aiu Modifica- tions were also necessary to some press decks in order to provide better sealing, thereby allowing operation at reduced fan speeds. Performance Data Acquisition As a part of the VOC control system, process parameters are monitored by permanent instrumentation. However, the existing system has no provisions for data storage. Therefore, process parameters of interest to this study were recorded during the test period by a temporary data acquisition system. The system consisted of a data interface unit and a personal computer. A floppy disk and thermal printer provided for hardcopy data output and storage. Performance Results Table 1 shows the effect of the VOC control system on the flowrate of air through the four presses considered in this study and confirms that the system operated as expected during the data acquisition period. Measured airflow rates were close to the expected values, which represented a 71% decrease in airflow when compared to the precon- version values. Despite the decrease in airflow rates, the percentage LFL re- mained well within acceptable and safe values. Equipment Cost and Energy Savings This installation of a microprocessor control system enables the plant's exist- ing boiler to be used for VOC destruc- tion. James River determined that use of the existing boiler was the most cost- effective method of addressing their VOC emission control requirements. In addition, significant cost savings result from operation of the system because the quantity of collected air was signifi- cantly reduced. These savings include: Reduction in energy demand for dryer air heating due to reduced air exhaust rates. Recovery of thermal energy in press exhaust by using the exhaust as air for boiler combustion (presi exhaust averages 23°C above ambi ent air temperatures annually). Recovery of calorific value of VOCs incinerated in the boiler. Table 2 summarizes installed cost for the conversion project at the Jame! River plant. Annual energy savings an summarized in Table 3. Safety The control system incorporates sev eral safety features and interlocks, in eluding: LFL analyzer failure (flameout) de tection. High LFL level alarm and pres: shutdown. Loss of deck exhaust flow. No LFL analyzer failures occurred dur ing the data collection period, nor wen acceptable percentage LFL levels ex ceeded. Based on the review of the sys tern design and operating data, thesi safety features operated as intended. Conclusions This study shows that rotogravur printing operations can benefit from th microprocessor-based control techno ogy discussed in this report. Economi benefit accrues due to the reduction i process air exhaust volumes whic must be processed by a collection syi tern or an incinerator or heated by process dryer. The techniques used t monitor and control VOC concentn tions and to allow lower air volumes at broadly applicable to processes whic Table 1. VOC Collection System Performance Summary After conversion Press No. 3047 3049 3051 3052 rnor to conversion Exhaust flowrate scfm (l/s) 20,000 (9,378) 25,000 (11.723) 7,000 (3,282) 25,000 (11,723) 77,000 (36,106)' Expected exhaust flowrate scfm (l/s) 6,000 (2,813) 4,000 (1,876) 4,200 (1,969) 8,000 (3,751) 22,200 (10,409)" Measured exhaut flowrate scfm (l/s) 6,105 (2,863) 3,839 (1,800) 4,245 (1,990) 7,900 (3,704) 22,089 (10,357)a "Totals have been rounded off for consistency. ------- Table 2. Conversion Cost Summary1985 Dollars Category Total ($1000s) Control System 1. Microprocessor control system3 2. LFL Analyzers" Subtotal Engineering 3. Preinstallation analysis and system design Collection and Transport System0 t. Ducting and press modifications 5. Boiler modifications Subtotal Total 295 145 440 100 720 300 1020 1560 'Includes computer, pressure transducers, and drives. 'Includes two FID analyzers, eight-channel manifold, and sample pump. 'Items 4 and 5 are unique costs, required only because James River was ducting to a boiler. If the plant had an existing incinerator, then these costs would not be applicable. "able 3. Annual Fuel Energy Savings Air reduction Units savings 3tu x Jfl6 34,250 loules x JO9 36,727 Air preheat savings 12,670 13,364 Calorific value 24,930 26,296 Total 71,850 75,787 use heated air in the presence of sol- vents or other materials. The system re- duces plant operating and pollution control costs by reducing fuel required to heat the facility air or the air used in the process. The application of microprocessor technology studied at James River is an extension of the technology from metal coating (i.e., painting) application. This study proved that the technology is ap- plicable to the paper coating industry and can provide economic benefits through the reduction in energy re- quirements for a printing process. Al- though the amount of energy savings and the cost of plant modifications will be different for each application, energy savings, in most cases should offset the capital cost of the plant modifications within a short time. Additional reduc- tions in operating costs will also be real- ized due to the reduced airflows. A potential user of a microprocessor control system should review the re- sults of this study to assess if similar energy and emission control benefits are possible in other applications of in- terest. In general, any application where airflows are used to carry away VOCs could be improved through active con- trol of both airflow rates and VOC con- centrations. Depending on the applica- tion, the b*st cleanup approach may be: Corr4in'stion in a dedicated inciner- ator. Combustion in an available plant boiler. Collection in a VOC recovery facil- ity. The best choice in a given situation will depend on the VOC quantities, airflow rates, plant layout, other plant equip- ment, energy costs, and permitting re- quirements. ------- D. Rosen andM. Wool are withAcurex Corporation. Mountain View, CA 94039. Charles H. Darvin is the EPA Project Officer (see below). The complete report, entitled "Microprocessor Control of Rotogravure Airflows." (Order No. PB 86-230 075/AS; Cost: $11.95. subject to change) will be available only from: National Technical Information Service 5285 Port Royal Road Springfield. VA 22161 Telephone: 703-487-4650 The EPA Project Officer can be contacted at: Air and Energy Engineering Research Laboratory U.S. Environmental Protection Agency Research Triangle Park. NC 27711 United States Environmental Protection Agency Center for Environmental Research Information Cincinnati OH 45268 Official Business Penalty for Private Use $300 EPA/600/S2-86/068 ------- |