United States
 Environmental Protection
 Agency
Air and Energy Engineering
Research Laboratory
Research Triangle Park NC 27711
 Research and Development
EPA/600/S7-85/013 July 1985
Project  Summary
Evaluation and  Demonstration of
Low-NOx Systems for  TEOR
Steam Generators: Final Report—
Field  Evaluation of Commercial
Prototype  Burner
G. England, Y. Kwan, and R. Payne
  The goals of this program were to
develop, demonstrate, and evaluate a
low-NQ burner for crude-oil-fired
steam generators used forthermally
enhanced oil recovery (TEOR). The
burner designed and demonstrated
under this program was developed
from design criteria established in
bench- and pilot-scale experiments.
This report describes the results of the
final phase of the program in which the
full-scale (16 MW() commercial proto-
type burner was successfully installed
and tested in the Kern County, CA, oil
fields on a conventional TEOR steam
generator. A 30-day continuous moni-
toring test demonstrated the capability
of the burner to continuously maintain
NOL emissions of 70 ppm with  CO
emissions below 50 ppm and particu-
late emissions below 0.23 g/dscm.
Detailed emission measurements also
showed negligible emissions of organic
species, including EPA priority pollut-
ants.  Thermal efficiency of the steam
generator was similar  to that prior to
the low-NOg burner retrofit and was
within the normal range for conven-
tional steam generators. The mechani-
cal performance of all major burner
components was satisfactory-

  This Project Summary was deve-
loped by EPA's Air and Energy Engi-
neering Research Laboratory, Research
Triangle Park, NC, to announce key
findings of the research project that is
fully documented in a separate report of
the same title (see Project Report order-
ing information at back).

Introduction
  Enhanced oil recovery processes are
applied to oilfield production in order to
extract heavy, viscous crude oil and tar
sands which cannot otherwise be pro-
duced. A significant fraction of total U.S. oil
reserves require application of enhanced
oil recovery in order to be realized. Ther-
mally enhanced oil recovery (TEOR)
involves injecting wet steam which is typi-
cally produced by combusting crude oil in
oilfield steam generators ranging in size
from 7 to 15 MW capacity. More than
90 percent of all oilfield steam generators
in the U.S. are in California, about one-
third of which are in Kern County. About
one-third of the produced crude oil is con-
sumed by the steam generator, amount-
ing to over 200,000 barrels (nearly 32
million  liters) of crude oil consumed per
day at full capacity.
  The crude oilsfired in these steam gen-
erators are typically high in nitrogen (0.8
to 1.0 percent) and sulfur content. Com-
bustion of these fuels leads to high levels
of N0xand SOxemissions unless preven-
tative measures are taken. The contribu-
tion of fuel-bound nitrogen to NOX emis-
sions from fuel oil  combustion is well
documented. A survey of conventional
TEOR steam  generators in Kern County
showed that uncontrolled NOX emissions

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ranged from 160to 825 ppm (corrected to
3 percent 02), depending on operating
conditions and design variables, with an
average emission level of about 325 ppm
at an average excess oxygen level of 4.5
percent. These high emission levels and
deteriorating air quality have prompted
state and local legislation regulating NOX
emissions from TEOR generators, which
threatens  to limit oil production unless
NOX control methods are applied.  For
certain new or modified stationary sour-
ces (including  TEOR steam generators)
these regulations require application of
the Best Available  Control Technology
(BACT) or the Lowest Achievable Emis-
sion Rate (LAER) to control the emissions
of any air contaminant or precursor for
which  there is a  national ambient air
quality standard (including NO,). Addi-
tionally, NOX emissions from alt steam
generators are currently limited to 130
mg/MJ (about 225  ppm, corrected to 3
percent oxygen).  Further reductions to
108 and 60 mg/MJ (about 190 and 105
ppm) may be required if ambient NO2
concentrations  exceed certain  trigger
levels.  NOX control techniques including
Iow-N0x burners, postflame NH3 injec-
tion,  or  other  postflame treatment
methods (e.g.,  selective catalytic reduc-
tion) have  been considered in order to
comply with regulations. Enhanced  oil
recovery operations are  projected  to
expand in  Kern County through 1995.
The level of N0xcontrol required to meet
both growth and air quality goals has typ-
ically been difficult to achieve with avail-
able  technology  while  maintaining
acceptable CO and particulate emissions
as well as practical flame conditions in
the steamer.
  This report describes the final phase of
a program which addresses the need for
advanced NC^ control technology for oil-
field steam generators. A full-scale (15.7
MW,) burner system has been developed
and tested, the concept for which was
based  on  fundamental  studies. The
design development phase of this pro-
gram has been extensively documented.
  The full-scale burner was constructed
and tested in an experimental test fur-
nace prior to being retrofitted to  a field-
operating  steam generator. This report
describes the retrofit and testing of the
burner on a conventional steam genera-
tor firing heavy crude oil in Kern County,
CA. The emission goals of the program
were: (l)todevelop to commercial scale a
low-NC^ heavy fuel oil burner;(2)to dem-
onstrate a  full-scale burner system for
use either as a retrofit or in new units; (3)
to evaluate the system in the field over a
prolonged period of time; (4) to achieve
NOX emissions less than 85 ppm and CO
less than 45 ppm with low smoke/partic-
ulate  emissions and acceptable  flame
shape; and (5) to  ensure acceptance of
the technology by the  industry.  All of
these goals were achieved.

Concept Background and
Development
  Combustion-generated NOX emissions
can be reduced by combustion modifica-
tion techniques which involve staging
the heat  release process.  Techniques
such  as flue gas  recirculation strive to
control NO formed from molecular nitro-
gen (thermal  NO) by suppressing peak
flame temperature, and are only partially
effective with nitrogen-containing fuels.
NO formation from nitrogen in the fuel
(fuel NO) is very sensitive to reactant stoi-
chiometry,  and  can  be  significantly
reduced  by initially  burning the  fuel
under fuel-rich conditions. Staged com-
bustion, therefore involves  creating  a
fuel-rich zone  to  promote formation of
molecular nitrogen from the nitrogen
species (HCN,  NH3, NO) evolved as the
liquid fuel  decomposes, followed by  a
fuel-lean zone  optimized for minimum
NO formation.
  The mechanisms controlling NOX for-
mation during  staged combustion were
identified in a  previous study for liquid
fuels ranging from distillate and residual
oils to alternative coal- and shale-derived
oils. The key parameters were first-stage
stoichiometry, thermal environment, and
residence time. NOX was  relatively
insensitive to second (burnout) stage
parameters. These bench-scale studies
showed that under optimum staged con-
ditions,  NOX emissions below 100 ppm
were  possible and were  independent of
fuel nitrogen content.
                     Refractory
                      Lining
  Based on the results of the bench-scale
studies,  prototype combustors were
designed and tested at 2 x 106 and 10 x
106 Btu/hr  to further  develop  scaling
criteria for the design of a full-scale (60 *
106 Btu/hr) burner. These pilot/scale
tests confirmed that a staged combustion
system could be designed and scaled
over a 150:1  range which is capable of
achieving less than 85 ppm NO (at 3 per-
cent O2) firing high-nitrogen residual  oil,
with low  CO and smoke emissions.

Burner  Design
'• Figure  1 shows the full-scale  burner.
Optimizing both  the fuel-rich and fuel-
lean stages is achieved  utilizing  a physi-
cally separate first-stage chamber,
formed by a 2.1 m I.D. horizontal  cylinder
which is  refractory lined  and recupera-
tively cooled to  maintain first-stage
temperature; the exterior of the chamber
is also insulated to prevent heat loss. The
recuperative design reduces thermal
inertia and thermal stresses developed
during transient (start-up and shutdown)
operation by employing a relatively thin
layer  of  refractory.  Substantial  primary
air preheat is developed, which enhances
full vaporization near the fuel injector.
  A commercial air register, ignitor, and
fuel gun are used in the primary  ignition
zone. The atomizer is a twin-fluid
internal-mixing atomizer using steam for
atomization.  Primary throat diameter
was scaled  up from  the  pilot-scale
burners on the basis of constant velocity.
The  exit  diameter  of the chamber is
reduced  to  provide a first-stage exit
velocity of about  50 ft/sec (15  m/sec)
while reducing radiative heat losses from
the first stage.
  Secondary air  is admitted  at the
chamber exit through discrete ports
oriented  parallel to and normal to the
                                                       Secondary
                                                        Air Inlet
                                I i \  II T~I
Figure  1.   Full-scale commercial prototype burner design.
                                                               Steam
                                                              Generator
                                                               Radiant
                                                               Section

-------
burner axis. The distribution of secondary
air can be varied to provide some degree
of control  over  second-stage mixing.
Testing  on the bench and  small pilot-
scale systems had shown that emissions
were insensitive to second-stage mixing
and excess oxygen level; however, at 2.9
MWt, results suggested  that these  par-
ameters may have greater influence on
emissions  and flame shape in larger
systems.
  The burner is equipped with a hybrid
electropneumatic control system for  nor-
mal ignition sequences and load modula-
tion. A programmable controller controls
first-stage stoichiometric ratio  and
second-stage  excess oxygen level for
minimum NOX emissions. The hybrid ap-
proach was selected for the reliability and
easy field maintenance of a pneumatic
system,  plus the flexibility and more  pre-
cise  control possible with a programma-
ble electronic controller.

Field Retrofit
  After the preliminary burner eval-
uation was completed in the test furnace,
the burner was transported to the  host
steam generator site in Kern County. The
burner had undergone about 131 hours
of operation during the preliminary eval-
uation, and first-stage  parameters  had
been optimized.
  The retrofit task of the demonstration
program involved selecting an existing
steam generator typical of  those  cur-
rently in operation to host the demonstra-
tion, transporting the burner to the  host
site, removing  the existing burner hard-
ware, and installing the prototype burner
hardware and controls. TEOR steam gen-
erators are relatively simple in construc-
tion  compared  with boilers, and utilize a
single-pass drumless design. The radiant
section is formed  by a horizontal,
refractory-lined steel cylinder, with the
burner at one end and an exhaust tran-
sistion leading to a convective econom-
izer  section at the other end. Steaming
tubes extend axially and are supported
near the refractory on tube hangers
around the generator circumference. The
entire unit, with  feedwater pump  and
controls, is normally skid-mounted  and
shop-assembled and is shipped by rail car
or truck to the installation site.
  Retrofit installation of the Iow-N0x
burner onto the host steamer required
replacing the refractory-faced front  wall
of the radiant section,  lengthening the
foundation and skid to accommodate the
length of the burner, extending plumbing
and  electrical wiring, and installing  sup-
plementary controls (e.g., programmable
controls, additional limit switches and
relays, and oxygen probe). Revised oper-
ating procedures to accommodate heat-
up and cooldown of the refractory lining
were also developed. Following comple-
tion and shakedown of the retrofit, test-
ing was initiated.

Field Test Results
  The steam generator was field tested in
three  phases: (1) optimization, (2)
detailed characterization, and (3) 30-day
evaluation.
  The purpose of the initial test series
was to optimize the burner operating
parameters to achieve safe start-up and
shutdown, acceptable flame characteris-
tics in the steam generator radiant  sec-
tion,  and low NO, CO, and smoke
emissions. The steam generator  was
gradually brought to full load on crude oil.
Initial  emission measurements were
consistent with results obtained in the
test furnace. However, at full load, flame
impingement on the walls of the radiant
section near the burner was encountered
(Figure 2). The flame  shape was much
wider and shorter compared to that
obtained in the test furnace, most likely a
result of smaller furnace diameter in the
steam generator.
  The  initial degree of control over
secondary air injection was not sufficient
to produce an acceptable flame, so other
modifications were considered. Although
a considerable body of  literature des-
cribes the behavior of confined double-
concentric jets in  both nonreacting  and
flame environments, there is little infor-
mation for highly confined systems sim-
ilar to the present burner/furnace
combination.  The multijet method of
secondary air addition also added
another degree of uncertainty in attempt-
ing to design the  optimum modification
by classical methods. A very brief series
of 1/5-scale, cold isothermal modeling
tests were therefore conducted using an
existing flow modeling facility in order to
evaluate  the  potential effectiveness of
the proposed modifications.
  The hardware for the 1/5-scale model
was geometrically scaled. Secondary air
jet velocity was held constant while pri-
mary flowrate exit velocity was reduced
to maintain the same momentum ratio as
at full scale. The flow pattern was visual-
ized with plane illumination and injection
of soap  bubbles using a commercial
neutral-buoyancy bubble generator. Mix-
ing patterns were determined by tracer
concentration measurements.
  The baseline configuration was evalu-
ated first to  determine  whether the
approach  to  scaling  would  produce
results similar to field observations. The
flow patterns in the model and full-scale
steamer appeared to be similar, charac-
terized by a strong external recirculation
zone near the burner  exit, rapid expan-
sion of the primary jet toward the wall,
and a lazy central recirculation zone. The
point where the boundary of the primary
streams reached the wall  in the model
correspond approximately to the point
where flame impingement had occurred
in the actual steam generator. The appar-
ent spreading angle  of the primary jet
boundary was about 20 degrees (half-
angle). The model also indicated that pri-
mary fluid was rapidly entrained into the
secondary jets and external recirculation
zone,  very near the burner exit. Overall,
the results obtained with the model in the
baseline  configuration  appeared  to
represent conditions  observed  in the
steam generator.
  Figure 3 shows model results for base-
line conditions and for two modifications
considered for the full-scale burner. The
first modification (3b) involved decreas-
ing the first-stage exit diameter. The pro-
posed diameter reduction increased the
primary to secondary jet momentum ratio
from 0.35 to 0.56. The resulting flow
pattern showed that the point where the
primary jet reached the wall was moved
50 percent farther downstream, with an
apparent spreading angle of 15 degrees.
Velocity in the external recirculation zone
was somewhat reduced, and the central
recirculation zone disappeared entirely.
                                                                Tube Hangers
Impingement
Region
iT^Jf
™ ^^
^^^(LjEi^
^•7 ""
V|
-------
 (a) Initial Configuration
                                                                      Tube
                                                                      Hangers
(b) Modification 1: Reduced   (c) Modification 2: Same as
Exit Diameter              Modification J  Plus
                         Increased Secondary
                         Nozzle Diameter
Figure 3.   Effect of changing primary and secondary jet momentum on mixing and flow
           patterns in cold isothermal model.
The  mixing profiles  indicated that  the
entrainment of primary fluid toward the
walls near the burner was significantly
reduced. Downstream of the region near
the exit, both streams appeared to be well
mixed, although downstream conditions
in the model may not accurately repres-
ent full-scale conditions.
  A second field modification considered
was  to remove  inserts from the axial
secondary air  ports, thereby enlarging
the port area and reducing the momen-
tum  of the secondary jets.  Figure 3c
shows the flow  and  mixing patterns
obtained with  both modifications simu-
lated in  the  model. This combination
resulted  in a  primary to secondary jet
momentum ratio  of 0.99. Reduction of
the  secondary jet momentum further
reduced the apparent spreading angle of
the primary fluid  boundary to about 13
degrees, and  significantly reduced  the
primary fluid concentration at the walls
of the model near the burner exit. In spite
of the  delayed  mixing  between  the
streams  near  the burner, good mixing
was  still achieved at a distance about
equivalent to the  midpoint of the steam
generator, as shown by the region of 0.7
primary fluid concentration.
  The  results  of  the isothermal model
tests indicated that entrainment of pri-
mary combustion products toward  the
furnace walls near the burners could be
reduced or delayed by modifying the exit
                geometry. The rationale for selecting one
                of the modifications over the others was
                based on interpretation of the isothermal
                model  results  as well as engineering
                judgement based on experience. Reduc-
                ing  the  primary  zone  exit  diameter
                appeared to offer reasonable potential for
                reducing entrainment without adversely
                affecting downstream mixing. Addition-
                ally, if the result of this modification was
                not satisfactory, the secondary air ports
                could be enlarged afterward. Since this
                appeared to be a reasonable  and cost-
                effective approach, a temporary sleeve of
                low-grade refractory bricks was installed
                in the primary exit to increase the velocity
                of gases at the first-stage exit by 47 per-
                cent. The secondary air  ports were not
                changed.

                Burner Optimization
                  The second  series of  burner shake-
                down tests showed that the modification
                had been successful in eliminating the
                flame  impingement problem completely
                with all 16 secondary air ports wide open.
                The visible flame was  significantly nar-
                rower and slightly longer than the origi-
                nal  flame.  The  center  of the  flame
                appeared clear with no signs of smoke or
                central recirculation zones. Flame shape
                was similar to the region in  Figure 3b
                bounded by the  isopleths of 0.6 to 0.7
                primary fluid  concentration. Overall
                flame  length was  about 5.5  to  6.1 m
(between the third and fourth  rows of
tube hangers).  The "tail" of the  flame
occasionally  licked  the  steam tubes;
however, this was considered minor and
did not raise concern over tube or refrac-
tory life. Since the flame shape produced
by the first modification was considered
adequate, no attempts were necessary to
further improve flame shape, and burner
optimization tests were initiated.
  Figure 4 shows NO, CO, and smoke
emissions from the steam generator fir-
ing at 54 x  1Q6 Btu/hr after optimization
of second-stage flame shape. Data are
shown versus first-stage stoichiometric
ratio for two excess oxygen levels. The
fuel was Kern Front crude oil (Table 1).
Minimum NO levels were between 55
and 65 ppm (corrected to 3 percent oxy-
gen). CO and smoke emissions were also
low at the optimum stoichiometry; how-
ever, below the optimum stoichiometry,
smoke was slightly higher for 2 percent
excess oxygen  than at 3  percent. This
behavior was attributed to second-stage
mixing; however, since conditions  below
the optimum stoichiometry do not repres-
ent normal operation, no further optimi-
zation   was required.  NO  and  CO
emissions  were  insensitive  to excess
oxygen. It should also be mentioned that
the measured CO emissions were near
the detection limit  of the continuous
(non-dispersive  infrared)  analyzer and


  Table 1.    Properties of Kern Front Crude
            Oil Used in Full-Scale Burner
            Field Evaluation

                           Kern Front
                             Crude
	Oil
  Ultimate Analysis, wt %
    Carbon                     85.42
    Hydrogen                   1088
    Nitrogen                     0.83
    Sulfur                        1.05
    Ash                         0.03
    Oxygen {by difference)           1.79
                              100.00

  Specific Gravity (@ 15°C)        0 978

  Viscosity
    SSU @ 140°F               2,450
    cp @ 60°C                    518

    SSU@210°F                 274
    cp @ 99°C                     58

  Heat of Combustion
    Btu/lb, Gross               18.310
          Net                   —

    kJ/g, Gross                  42.6
        Net                     —

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  150
I
•7$
o
  100
   50
           Excess Oi(Dry)

           A 2.0 Percent

           O 3.0 Percent
                                       15
                                       O
                                       ^
                                       00
100
                                      8 BO
                                          0
                                            10

                                             8
    0.5             0.6             0.7      0.5

                           First-Stage Stoichiometric Ratio

Figure 4.   Field test results: NO, CO,  and smoke emissions
           optimized burner configuration (54 x /0B Btu/hr).
 may represent interference by C02. Mea-
 surements of COby gaschromatography
 indicated that true levels were below 1
 ppm.


 Long Term Evaluation

 Particulates
   Based on the results of the optimiza-
 tion  tests, ideal  operating  conditions
 were programmed into the burner control
 system. A more detailed emission char-
 acterization was performed at the opti-
 mum full-load operation point, including
 paniculate mass loading and size distri-
 bution, organic compounds, and manual
 (reference method) gas analyses, in addi-
 tion to the normal continuous gas anal-
 yses. Total paniculate mass loading was
 determined three ways (EPA method 5,
 cascade impactors,  and  modified EPA
 Source Assessment Sampling System).
 Results from five measurements ranged
 from 23 x  1Q3 to 46 * 103 /L/g/m3 (0.010
 to 0.020 gr/dscf) of flue gas. This is the
 level expected for quantitative conver-
 sion of ash in the fuel. Visual inspection
 of paniculate catches indicated that no
 carbonaceous paniculate was present.
 Figure 5 shows paniculate size distribu-
 tion, for the optimum full-load operating
 condition.  Most of the paniculate is very
 fine,  with  approximately 65  percent
.below 1 um.
                                                          0.6
                                                                           0.7
                                                       from steam generator with
            Organic Emissions
              Emission of organic  compounds was
            also determined. Total (volatile, semi-
            volatile, and non-volatile) organic com-
            pound  emissions  were  below  0.3
            mg/dscm). Emission of priority pollu-
            tants was between 6 and 14 pg/dscm.
            Although no Federal standard has been
            established for emission of organic spe-
            cies, these levels are considered low for
            oil-fired sources. Emissions of NH3and
            HCN were also low, below 1 ppm.

            30-Day Test
              NOX C0?, CO, S02, and O2were moni-
            tored continuously in the steam genera-
            tor  exhaust during  30-day test under
            another EPA contract. Complete results
            are not yet available. Flue-gas oxygen
            concentration averaged about 2.8 per-
            cent (dry-basis)  during this period,  in
            agreement with the control system set
            point.
              NOXemissions averaged about 69 ppm
            during   the  9-day  period  for  which
            detailed data were  available,  and CO
            emissions remained below 50 ppm. N
            emissions typically ranged between 5
            and 75 ppm (corrected to 3 percent 02).
              SO x emissions were measured during
           • this period. SO2 concentration ranged
                                         8
                                        Q
                                        .a
                                        00
     1
   0.8

   0.6

   0.4
                                           0.2
                                           0.1
                                                     Total Mass Loading:
                                                    34 x rO3 ijg/m3 f0.015 gr/dscf)
                                                                    i
                                             0.01
                                       Figure 5.
10          50         90

 Cumulative Percent Undersize
                                                                                                    99
                                                                       99.99
          Field test results: paniculate size distribution (by cascade impactors) under optimum
          conditions.

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between about 520 and 650 ppm (cor-
rected to 3 percent OJ and averaged
about 580 ppm. These  levels are in the
range expected based  on 100 percent
conversion of the sulfur in the fuel.
  Preliminary  evaluation  of  results
obtained over  the entire 30-day period
indicates that these results are typical of
the entire period.

Efficiency
  Thermal efficiency of the  host steam
generator was determined  before and
after the commercial prototype burner
was retrofitted. Table 2 shows thermal
efficiency determined  by  input/output
measurements and by heat loss. In gen-
eral, the heat loss method is considered
to be  more accurate  because of the
smaller errors involved with each mea-
surement. Unrealistically high efficiency
determined by the input/output method
is most likely due to errors in the mea-
surement of steam quality. Data obtained
by the host operators prior to the burner
retrofit showed heat loss efficiency rang-
ing from 83.6 to 87.8 percent (neglecting
unmeasured and radiation  losses). Aver-
age heat loss  efficiency was 85.5 per-
cent. Data  obtained during  the burner
tests prior  to  the 30-day test showed
average heat-loss efficiency of 86.1  per-
cent. Thus  it can be seen that thermal
efficiency was  similar before and after
the burner retrofit.

Mechanical Performance
  After the 30-day test, the burner was
inspected to determine the mechanical
condition of each major component. The
burner had undergone over 1600 hours
of testing and was cycled 20 times, 7 of
which  were  unforeseen  shutdowns,
including three power outages. Addition-
ally the burner had survived the rigors of
being transported 480 km from the EER
test site in  El Toro, CA, to the host steam
generator site.
  The overall mechanical condition of the
burner was very good  after the 30-day
test. A key area  of concern was how well
the refractory lining had survived the 30-
day test, especially the numerous ther-
mal cycles. Inspection  of the refractory
lining showed that all refractory, includ-
ing  the primary burner throat, was  in
excellent shape, except for  a small sec-
tion of brick on the  front wall and the
temporary sleeve in the first stage exit.
These  relatively minor  problems have
been corrected. The burner control sys-
tem successfully maintained emissions
of criteria pollutants within  the program
goals for the duration of the 30-day test
without  operator  supervision.  This
proves the practicality  of  maintaining
minimum NOxemissions through control
of first stage stoichiometry. Minor excur-
sions in NOxoccurred due to drift in the
fuel-flow meter output as a  result of
changes in  ambient temperature. The
output of the fuel flow meter is utilized by
the programmable controller to maintain
constant first  stage  stoichiometry. The
drift problem  has also been  corrected.
Performance  of all  other control ele-
ments was satisfactory.
  The mechanical condition and opera-
bility of the burner were generally satis-
factory at the end of  the 30-day test.

Scaling and Applicability
  Criteria developed in bench- and pilot-
scale tests were applied to the design of
the full-scale prototype Iow-N0x burner.
These criteria: (1) optimized of "the fuel-
rich first stage conditions for maximum
conversion of fuel-bound nitrogen to N^
and (2) optimized second-stage condi-
tions for minimum  thermal  NO and
smoke formation. The key design criteria
are:
1.  Fuel Injection
    -  High quality atomization.
    -  Premixed fuel/air.
    -  Minimal heat  extraction to maxi-
       mize fuel vaporization rate.
2.  First-Stage Fuel-Rich Zone
    -  Stoichiometric  ratio  approxi-
Table 2.    Thermal Efficiency of Host Steam Generator
                                               A.  Prior to Burner Retrofit
Date
9/2/82
1 1/22/82
12/6/82
1 1/4/83
8/16/83
5/19/83
Heat
Release (a)
MWt
15.7
18.4
16.6
15.7
12.1
16.7
Excess O2
wet basis
3.7
3.1
2.8
2.8
2.3
2.9
Steam (b)
Quality
66
82
68
75
81
73
Thermal (c)
Efficiency
80
82
80
86
91
93
Flue Gas
Exhaust
Temperature
°C
177
259
160
232
215
232
Thermal (c)
Efficiency
87.1
83.6
87.8
84.8
85.1
84.8
 avg
                        15.9
2.9
                                                         74
                                                                        85.3
                                                                                         213
(a) per barrel of crude oil
(b) by electrical conductivity
(c) input/output - determined by host
(d) heat loss - determined by EER according to ASME method. Estimates were used where measurements were not taken.
                                                                 85.5
B. After Burner Retrofit


Date

1/5/84
1/7/84
1/7/84
1/9/84
avg


Time

1225
—
0725
0750
—
Heat (a)
Release
MWt

15.7
15.7
15.7
15.7
15.7
Excess
o.
%. dry

2.9
2.9
2.9
3.0
2.9
Steam
Quality (b)
%

83
73
83
84
81
Thermal
Efficiency (c)
%

103
87
97
95
95.5
Flue Gas
Exhaust
Temperature
°C
196
204
210
234
211
Thermal
Efficiency (d)
%

86.4
86.4
86.2
85.4
86.1

-------
       mately 0.7 to minimize total fixed
       nitrogen (TFN) concentration.
     -  Residence time in excess of 400
       msec  to  allow  sufficient TFN
       decay.
     -  Control of heat loss to produce a
       first-stage temperature in excess
       of 1427°C to promote rapid con-
       version of fuel nitrogen fragments
       to molecular nitrogen.
 3.   Second-Stage Air Injection
     -  Partial  quenching  to  minimize
       thermal  NO  formation  in  the
       second stage.
     -  Refractory choke to prevent back-
       mixing and reduce heat loss.
     -  Intermediate  to  rapid  second-
       stage mixing  to minimize smoke
       formation  and  control  flame
       shape.
   Full-scale  burner  tests,  firing high-
 nitrogen heavy oils in the experimental
 furnace and in the oilfield steam genera-
 tor, confirmed that  the  design criteria
 could be applied to full-scale hardware to
 produce the  expected emission results.
 Figure 6 compares NOX emissions from
 bench-, pilot-, and full-scale tests versus
 first-stage residence time. The results
 represent a 750:1 range in scale. Below
 approximately 0.6 seconds, NOX emis-
 sions from the tunnel furnace are slightly
 higher than from the pilot-scale systems
 due to higher heat losses from the first
 stage associated with the smaller scale.
   Data from  the full-scale  system indi-
 cate that increasing residence time
 above 0.6 seconds is  less beneficial. This
 asymptotic behavior may indicate a shift
 in the controlling mechanisms from first
 to  second stage  processes at very low
 NOX levels. Earlier pilot-scale tests firing
 nitrogen-free  fuels  (distillate  oil, pro-
 pane) produced minimum NOX levels of
 about 40 to 50 ppm  from the optimized
 burner configuration, which was  attrib-
 uted to second-stage  thermal NOxforma-
 tion. Although full-scale burner perfor-
 mance  indicated that emissions exhi-
 bited some sensitivity to second-stage
 parameters (mixing,  confinement), this
 sensitivity is much less severe than typi-
 cally encountered in conventional sys-
 tems: the greatest impact is  on  flame
 shape.
   Figure  7 compares NOX emissions
 from the  prototype burner to  field test
 data for conventional 50 x 106 Btu/hr
 steam generator  burners and  for other
 current N0xcontrol technology. Average
 NOxemissions from conventional bur-
 ners range from about 230 to  280 ppm
 over the range of excess air investigated.
, By comparison, emissions from the pro-
 o.
 0.
 -3
 O
 9.
 x
 O

 1
 5
 5
 §
    140
    120
    100
80
60
     40
     20
      A
      O
      O
Tunnel Furnace 70 x 103 Btu/hr (21 kW)

Small Prototype 3x10* Btu/hr (1 MW)

Intermediate Prototype 10 x 10* Btu/hr (3 MW)
Commercial Prototype 55 x 10e Btu/hr (16 MW)—Test Furnace
Commercial Prototype 54 x /O6 Btu/hr—Field Test
                 0.2        0.4        0.6         0.8         1.0

                           First-Stage Residence Time, seconds
                                                                 1.2
Figure 6.
       Comparison of A/0X emissions from bench-, pilot-, and full-scale prototype burner
       designs.
totype low NOX burner are about 65 ppm
and  insensitive to excess  oxygen. This
represents a 77  percent reduction over
average NOX emissions at 3 percent ex-
cess oxygen, without adverse impact on
other pollutant emissions. Other low-
NOX burner data  indicated that the main
benefit of the  burners tested was
improved operability at lowexcessair
levels. Recent low-NOxburnertechnol-
ogy has shown that significantly reduced
NOX emissions can be achieved by de-
layed fuel/air  mixing  within the steam
generator in combination with  flue gas
recirculation; however, the impact of the
result ing flame conditions on furnace
integrity has not been fully evaluated:
some low excess oxygen conditions can
result in high CO and  smoke emissions.
NOX reduction by postflame NH3 injection
into the steam generator radiant section
has produced N0xemission levelscom-
parable to those achieved in this pro-
gram. Test results indicated that it was
difficult to maintain optimum NH3 inject-
ion conditions over extended periods
because of changes in furnace heat
transfer caused by tube fouling in the con-
vective section.  This could lead to NH3
breakthrough or higher N0xemissions. If
the practical problems can be resolved,
these developing technologies may prove
to be key to NOX  reduction.
                                   Conclusions
                                     The prototype Iow-N0xburner which
                                   was developed in this program demon-
                                   strates the applicability of the general
                                   design criteria developed in bench- and
                                   pilot-scale studies. Results of the 30-day
                                   test demonstrated that all program emis-
                                   sion goals were met for an extended
                                   period of time with no adverse impact on
                                   steam generator performance. Following
                                   the test program, the host management
                                   requested that the burner remain
                                   installed on the steam generator. Burner
                                   performance  will be monitored to deter-
                                   mine long-term performance and estab-
                                   lish operating and maintenance costs.

-------
     500
     400
  §;  300
 0
     200
     ;oo
                      \             \
          50 x 10* Btu/hr Steam Generators
                                              Conventional Burners
                                              A verage of 64 Tests
                                              ± Std. Dev.
              Low-N0« Burners
                                            Low-NOi Burner
                NH3 Injection •
                                                  This Work
                                   I
        0             12345

                               Excess O2 (Dry), percent

Figure 7.   Comparison of prototype burner performance to conventional technology and
           current low-NOi burner technology.
  G. England, Y. Kwan, andR. Payne are with Energy and Environmental Research
    Corp.. Irvine, CA 92714.
  Michael C. Osborne is the EPA Project Officer (see below).
  The complete report, entitled "Evaluation and Demonstration ofLow-NOi Burner
    Systems for  TEOR Steam  Generators: Final Report—Field Evaluation  of
    Commercial Prototype Burner," (Order No. PB 85-185 874/AS; Cost: $ 17.50,
    subject to change) will be available only from:
          National Technical Information Service
          5285 Port Royal Road
          Springfield,  VA 22161
          Telephone: 703-487-4650
  The EPA Project Officer can be contacted at:
          Air and Energy Engineering Research Laboratory
          U.S. Environmental Protection Agency
          Research Triangle Park. NC27711
                                                                         U. S. GOVERNMENT PRINTING OFFICE: 1985/559-111/20612

-------
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