United States Environmental Protection Agency Air and Energy Engineering Research Laboratory Research Triangle Park NC 27711 Research and Development EPA/600/S7-85/020 Aug. 1985 Project Summary Field Evaluation of a Utility Dry Scrubbing System Gary M. Blythe, Jack M. Burke, David L Lewis, and Carol May Thompson This program was the first indepen- dent evaluation of a full-scale utility spray-dryer/baghouse dry flue gas desulfurization (FGD) system. The eval- uated system treats flue gas from a nominal 100 MW of coal-fired power generation. For the test program, two different coals were used as boiler fuels: one, a subbituminous coal and coke mixture with a nominal 1.2 percent sulfur con- tent; and the other, a 3.4 percent sulfur Illinois bituminous coal. The test program was conducted from July to October 1983. SO2 re- moval, participate emissions, sulfuric acid removal, and extensive process data were recorded. Low sulfur coal tests indicated that 75 percent SO2 re- moval was achievable in the short term at reagent ratios of 0.6 to 0.7, and 90 percent SO2 removal was achievable at a reagent ratio of about 0.8. An average removal of nearly 90 percent was achieved in short-term tests with high sulfur coal at reagent ratios of 1.3 to 1.4. Calcium chloride addition to the atom- izer feed slurry was found to reduce the lime addition requirements for high sul- fur tests by about 25 percent. This Project Summary was devel- oped by EPA's Air and Energy Engineer- ing Research Laboratory, Research Tri- angle Pack, NC, to announce key findings of the research project that is fully documented in a separate report of the same title (see Project Report or- dering information at back). Introduction This Summary discusses results from a program, the objective of which has been to acquire performance data on an operating, utility-scale, spray-dryer- based, dry FGD system. The system was evaluated primarily to determine SO-z and particulate removal performance and lime reagent consumption. The sys- tem chosen for evaluation is the Joy/ Niro Demonstration Unit, at the North- ern States Power Company (NSP) River- side Station in Minneapolis, MN. The Riverside system was chosen for this program because it is the first lime- based system in operation using a full- size (46-ft* diameter) spray dryer mod- ule. Testing was conducted with both low and high sulfur boiler fuels. The program was conducted for the Envi- ronmental Protection Agency's Air and Energy Engineering Research Labora- tory and for the Electric Power Research Institute under a cooperative funding arrangement. Project Description The project description includes that of the Riverside station and FGD sys- tem, a summary of the test program, and a discussion of the limitations of the Riverside system and how they have af- fected this evaluation. Site Description The Riverside generating station, op- erated by Northern States Power Com- pany, in northeast Minneapolis. The two units of interest on this project, No. 6 and No. 7, began operation in 1949. The combined generating power of Units 6 and 7 is rated at 98 MW. How- ever, the pulverized coal, wall-fired units were originally designed to fire an eastern bituminous coal. Recently, the units have fired a western (Sarpy Creek) subbituminous coal. A small amount (10 to 15 percent) of high sulfur coke is Readers more familiar with metric units may use the conversion table at the back of this Summary. ------- Flue Gas — From Unit 7 Flue Gas From Unit 6 U Spiral Grits Claesifter Unit 7 Stack ID Fan Unit 6 Stack ID Fan Slaking Water Lime Slurry Storage Trough Atomizer Feed Tank Figure 1. Flow diagram for Riverside dry FGD system. added to the subbituminous coal to im- prove its firing properties. The units can still be fired with high sulfur bituminous coal, and in fact were so fueled for 5 weeks of this test program. In 1980, a full-scale, Joy/Niro, spray- dryer/fabric-filter FGD system was in- stalled to treat the combined flue gas from the two units. The fabric filter was actually purchased by NSP because of limitations on the ability of existing ESP collectors to efficiently collect the ash from the western coal. The spray dryer system was installed by Joy/Niro under a cooperative agreement with the utility to serve as a full-scale demonstration of the capabilities of their dry FGD system. Figure 1 is a simplified flow diagram of the system. The spray dryer is 46 ft in diameter, with flue gas introduced both above the atomized spray in a roof gas disperser and below the atomized spray in a cen: tral gas disperser. A rotary atomizer is used, employing a 700 hp drive motor. The spray dryer was sized to treat flue gas corresponding to a 70 MW boiler load. This reduced sizing permitted sys- tem tests at greater than design flow rates. Note that, because Units 6 and 7 are over 30 years old, the flue gas flow rate at 70 MW is equivalent to the flue gas rate from about a 100 MW new unit. A new unit would experience much less air inleakage and operate at a much lower net plant heat rate than these units. The downstream fabric filter con- tains 12 compartments, in 2 rows of 6 compartments each. Because the fabric filter was sized to treat hot flue gas, it is actually oversized when the spray dryer is in operation because of the flue gas volume shrinkage which results from the reduced spray dryer outlet tempera- ture. Pebble lime reagent is slaked in a Joy/ Denver attrition slaker. A Joy/Denver ball mill is also available for lime slak- ing. Milk of lime, dilution water, and re- cycle solids are added to a mix tank at rates determined by a Honeywell pro- cess control computer. The mix tank ef- fluent is pumped to a separate atomizer feed tank. From the atomizer feed tank, slurry is pumped to a head tank at the top of the spray dryer. A pinch-type con- trol valve regulates the flow of slurry to the atomizer to maintain either a con- stant spray dryer outlet temperature or a constant approach to adiabatic satura- tion. When the system is operated to control S02 removal, the Honeywell process control computer calculates the amount of lime which must be added upstream at the mix tank to achieve the desired S02 removal. Recycle material is added at the mix tank at a rate re- quired to bring the mix tank solids level up to a set point, normally 35 weight percent solids. The recycle solids are collected from the spray dryer bottom dropout and largely supplemented by a ------- portion of the fabric filter catch. Testing Approach As described in the introduction, a pri- mary objective of the program was to quantify SO2 removal by the system. A continuous emission monitoring sys- tem (CEMS) was temporarily installed to quantify S02 removal. The CEMS in- cluded a DuPont Model 460 two-point extractive S02 monitor and a Thermox 02 monitor (sampling the spray dryer inlet and outlet ducts), and a Lear Siegler SM810 in-situ point-type S02 analyzer (installed in a short run of duct at the fabric filter outlet). A second Ther- mox 02 analyzer was mounted on the duct exactly opposite the Lear Siegler monitor. Other than SO2 removal data, lime consumption and other important pro- cess parameters were recorded as hourly averages for each test day. Lime consumption was measured primarily by determining the lime content of the milk of lime slurry introduced to the at- omizer feed mix tank. The flow rate of this slurry was continuously measured with a magnetic flow meter and re- corded by the Honeywell process con- trol system computer. Other methods of lime consumption measurement have included continuous quicklime weigh belt rate measurements, recording of daily quicklime trucklbad deliveries, and determination of the lime content and flow rate of the actual atomizer feed slurry. Enthalpy balances have been used to confirm agreement between slurry feed rate and flue gas flow mea- surements. In addition to quantifying S02 re- moval and lime consumption perfor- mance for the spray-dryer/baghouse system, determination of particulate re- moval performance for the system was also an objective. This performance was determined by manual sampling of flue gas streams for particulate concentra- tions, using EPA methods. Particulate loadings were measured at the spray dryer inlet, spray dryer outlet, and fabric filter outlet. Test Plan The test schedule is summarized in Table 1. These tests were conducted be- tween July 11 and October 8, 1983. The schedule shows three sets of conditions with low sulfur, Sarpy Creek coal/coke blend, and two sets with high sulfur Peabody Illinois coal. The Sarpy Creek ^coal/coke blend has a nominal sulfur "content of 1.1 to 1.2 percent and a heat- Table 1. Test Schedule and Desired System Operation Conditions" Fuel Sarpy Creek Coal/Coke Sarpy Creek Coal/Coke Sarpy Creek Coal/Coke Illinois Coal Illinois Coalb SO2 Removal Level, % 75 75 90 90 90 Fabric Filter A/C Ratio, cfm/ft2 2:1 2.3:1 2:1 2:1 2:1 "All tests planned to be conducted at at 18°F approach to adiabatic saturation, 35 weight percent solids in the atomizer feed slurry, a 70 MW daytime boiler load, a once-per-hour baghouse cleaning frequency, and an attrition-type slaker. bCalcium chloride addition tests. ing value of 9000 Btu/lb. New Source Performance Standards for utility boil- ers would require 75 to 80 percent SO2 removal for boilers firing a fuel with this sulfur and heating value. In some locali- ties, state or local regulations might re- quire as high as 90 percent S02 removal with this fuel. Consequently, low sulfur tests were conducted at both 75 and 90 percent target S02 removal levels. Addi- tionally, some tests were conducted at a fabric filter air-to-cloth ratio higher than the nominal value of 2:1. Two sets of conditions were tested with the high sulfur coal. The coal was an Illinois No. 6 coal with a nominal 3.4 percent sulfur content and 10,700 Btu/lb heating value. Current New Source Per- formance Standards for utility boilers require approximately 90 percent S02 removal when coal of this sulfur content and heating value is burned. Conse- quently, only a 90 percent target S02 removal was tested with this high sulfur coal. The tests included baseline condi- tions of 90 percent removal with attrition-slaked lime and a second test run employing calcium chloride addi- tion for lime utilization enhancement. Chloride addition to enhance lime uti- lization in spray-dryer/baghouse FGD systems has been tested previously in bench- and pilot-scale systems, but this is the first test of chloride addition at a full-scale utility installation. The en- hancement effect is thought to occur be- cause of the deliquescent properties of calcium chloride. System Limitations Several system limitations combined to restrict the amount and the type of data that could be collected. First, as mentioned earlier, Riverside Units 6 and 7 are peaking units. As such, they are rarely operated in the winter and only operate part-time during July to Octo- ber. This part-time operation involves unit loads of 70 to 90 MW during week- day daylight hours, minimum load (30 to 50 MW) overnight during the week, and banking the boilers over the week- end. Although the FGD system was op- erated at desired S02 removal levels 24 hours per day, only about 12 hours per weekday of near full-load operation were available for evaluating FGD sys- tem performance. At the beginning of each 12-hour full-load period, the FGD system generally goes through a tran- sient period due to a large increase in boiler load. On Mondays, the unit must undergo a cold start-up. Although this cycling provides a severe test of the ca- pabilities of the system, it reduces the period of steady state operation at the desired S02 removal level over which lime reagent consumption can be mea- sured. Additionally, the Riverside system was the first utility-scale system de- signed and built by Joy/Niro as a demonstration unit. As the first unit built, the Riverside system has provided the opportunity to refine and modify de- sign features for subsequent systems. Thus, some specifics of the Riverside system are different from what will be found in later designs. An example of this is the slurry feed system, which has been modified for subsequent systems to provide quicker response to tran- sients such as load changes. At River- side, the slurry feed system has a resi- dence time of about 1.5 hours. This means that following an abrupt process change, such as a load change, it may take 3 to 4 hours for the slurry feed sys- tem to stabilize near steady-state condi- tions. ------- The impacts of the slurry feed prepa- ration system residence time are partic- ularly important at the Riverside station, as the normal station operation causes significant load changes at least twice per day. In fact, on some days during this test program, the unit load varied between 70 MW and 90 MW throughout the day. On these days, the unit never operated at one load long enough for the feed system to stabilize. On most other days, even if the load was steady all day, only 8 or 9 hours of the 12 hours of full load operation actually repre- sented steady-state conditions. Other aspects of the Riverside sys- tem's status as a demonstration unit af- fected the results of this program. For example, the system contains only one spray dryer module, while most utility systems will have multiple modules. In a multiple-module system, equipment problems which affect one individual module have a smaller impact on over- all system performance. Being a one- module system, equipment problems tended to cause the entire system to have to be shut down, or operated at conditions other than those desired. Also, because the Riverside system is a demonstration, rather than a commer- cial system, some individual compo- nents of the system have not been in- stalled with the redundancy that the vendor would likely install in a commer- cial system. These considerations have had a detrimental effect on both the amount of system downtime and the number of process-equipment-related upsets during the test program. A final consideration which has af- fectd the test program involves the re- cent history of the Riverside station. For nearly the first 2 years of operation, the FGD system was used as a full-scale demonstration and testing unit by the process vendors. During this time, Joy/ Nirohad responsibility for the operation of the system, even though NSP actu- ally provided operating personnel. Within the year prior to the test pro- gram, NSP had assumed responsibility for the operation of the FGD system. Im- mediately prior to the test program, the Units 6 and 7 boilers and FGD system were off-line for much of the winter and spring, as NSP does not need power production from these units during this time. During this long period of down- time, normal personnel turnover (pro- motions, retirement, transfers, etc.) re- sulted in a number of new operators rotating into the FGD system operating staff. At the start of the test program, then, the FGD system was being oper- ated for the first time in several months with a staff of operators having little previous experience with the FGD sys- tem. Early in the program, the operators tended to revert to conservative higher spray dryer outlet temperatures during any minor upset, such as soot blowing in the boilers. This would move the op- eration away from the desired condi- tions and would preclude acquiring de- sired steady state operating data. As the program continued, these excursions occurred much less frequently as the operators became more comfortable with operating at test conditions. Considering the previous discus- sions, it was not realistic to report avail- ability of the system, as the availability of the Riverside system would tell little about that of a commercial utility, multi- module, dry FGD system on a new base- loaded boiler. The combined effects of weekly cold start-ups, frequent load changes, little redundance, and a some- what undertrained operating staff at Riverside do little to promote a fair as- sessment of the potential availability of a commercial system. However, the general operation of the system was closely observed during the test program. Much of the downtime or off-condition operating time was due to problems specific to the Riverside sys- tem. Others appear to be more generic to dry FGD systems. These more generic problems are discussed in the report, as they are more likely to occur in other systems. Results The discussion of the program results is divided into two areas: Operational Results, which includes a qualitative discussion of the operation of the system during the test program; and System Performance, which includes preliminary S02 removal, lime con- sumption, particulate and sulfuric acid removal data, and solid waste charac- teristics. Operational Results In general, the equipment that com- prises the basis of the dry FGD system, the spray dryer and baghouse, were rel- atively trouble-free throughout the pro- gram. At the conditions tested, the spray dryer did not show evidence of potential problems (e.g., wheel nozzle pluggage, excessive buildup of solids on the walls, or formation of wet solids within the dryer). Some atomizer prob- lems were observed, but most of these | appeared to be caused by circum- stances specifc to the situation at River- side rather than being generic to the Joy/Niro system. These problems will be discussed further later in this section. The baghouse also operated well, with no significant bag/fabric related problems being observed. In this short-term test though, long-term ef- fects such as bag life or compartment wall corrosion rates could not be evalu- ated. Some problems were observed in four specific areas—the slurry feed sys- tem, the ash handling system, the ball mill slaker, and in atomizer protection. The system vendors may have ad- dressed these problems in system de- signs subsequent to Riverside, but the problems could be encountered in vir- tually any spray-dryer-based dry FGD system. Each of these areas is discussed below. Slurry Feed System In a recycle lime system, lime slurries containing up to 25 percent solids and recycle/lime slurries of 30 to 40 percent solids are commonly encountered. When dealing with slurries with a high solids content and high viscosity, prob- lems (e.g., plugging of pump suction lines, solids buildup on tank walls, plug- ging of in-line screens used to remove oversize material, and loss of flow when switching pumps) are commonly en- countered. Such problems were en- countered often at the Riverside sys- tem. Years of operation of wet lime/ limestone FGD systems have estab- lished means of dealing with such prob- lems. The quantities of these slurries that must be dealt with in a spray dryer system, though, are much smaller than what would be encountered in a wet system. At Riverside, typical atomizer feed slurry rates are 150 to 200 gpm. In a similarly sized limestone wet FGD sys- tem, the slurry recirculation rate could be as high as 40,000 gpm. While some of the slurry handling problems of a wet FGD system may still be encountered in a spray dryer system, they will occur on a greatly reduced size of equipment. This should make both problem solving and routine maintenance easier. An- other important point to be noted is that chemical scaling tendencies were not observed at Riverside. Ash Handling System In comparing the wet versus dry FGD t systems, the spray dryer system has a * ------- slurry feed system that deals with much lower flow rates for a given unit capac- ity, but the quantities of dry ash and FGD by-products that must be moved around the system are substantially greater than for a comparably sized par- ticulate collection device/wet scrubber system. The problem with solids handling which most frequently occurred at Riverside involved the baghouse me- chanical conveyors, blow pots, and the recycle bin rotary valve. Failures in any of these components could interrupt the flow of recycle material to the slurry mix tank, and cause the system to approach once-through operation. Ball Mill Slaker During this program, the ball mill slaker did not operate successfully for any extended period: the feed end of the slaker tended to plug with wet lime solids. While there are several possible reasons why the plugging continually occured, the actual cause was not iden- tified. The ball mill slaker problems at River- side appear to be somewhat site- specific (ball mill slakers have operated successfully elsewhere). In retrospect, the slaker might have run more success- fully at a higher water-to-lime ratio, re- sulting in a less viscous product slurry and less vapor release. However, in the attempts to run the ball mill slaker dur- ing the high sulfur tests in particular, the slaking water piping size did not allow operation at higher water-to-lime ratio at the lime slaking rates required. Dur- ing the high sulfur tests, lime slaking rates averaged approximately four times that required for the normal low sulfur fuel at similar unit load and per- cent S02 removal conditions. Atomizer Problems Although the atomizer motor, gear- box, and nozzle wheel were generally trouble-free, on several occasions prob- lems which could result in atomizer damage were observed. Two scenarios for potential damage were observed. One occurred when the unit was forced to run from the basic, or less sophisticated, control station of the computer control system while the more sophisticated supervisory station was undergoing repair. The control software at Riverside does not have full interlock protection for the atomizer when running from the basic station. . (Interlocks are software which automat- ically shut down the atomizer when Table 2. SO^ Removal Results, Low Sulfur Coal Average SO2 Removal, % 74 75b 89 Spray Dryer Removal, % _a 67 78 Fabric Filter Removal, % _a 8 11 Reagent Ratio 0.7 0.6 0.8 Recycle Ratio 13:1 14:1 11:1 "Not measured. Increased air-to-cloth ratio at fabric filter; other tests at normal air-to-cloth ratio. Table 3. S02 Removal Results, High Sulfur Coal Average S02 Removal, % 88 89a Spray Dryer Removal, % 72 62 Fabric Filter Removal, % 16 27 Reagent Ratio 1.3 1.0 Recycle Ratio 2:1 3:1 aHigh chloride concentration tests. given inputs that are indicators of prob- lems which might result in damage to the atomizer.) While running in this mode, a minor problem involving loose wires to the atomizer oil circulating pump occurred, intermittently shutting off the pump. However, the basic sta- tion only gave the control operator an alarm rather than shutting down the atomizer automatically. The atomizer continued to run for several minutes without oil circulation and sustained gearbox damage. The second scenario which could re- sult in atomizer damage was observed on more than one occasion: it involved feeding slurry to the atomizer wheel when it was not rotating. Since the non- rotating wheel has a much lower hy- draulic capacity than a rotating wheel, slurry fed to the standing wheel tends to overflow the wheel and can flow up the spindle to which the wheel is attached and enter the atomizer oil system. In such instances, the oil sump can be im- mediately emptied and flushed to avoid damage, but if the atomizer is operated before cleaning, the slurry in the oil can eventually cause gearbox damage. System Performance The results of S02 removal and lime consumption measurements during this test program are summarized in Tables 2 and 3. Table 2 summarizes the low sulfur coal SO2 removal results; and Table 3 summarizes those for the high sulfur coal tests. For several reasons, the SC>2 removal results from the program cannot be ex- pressed as 30-day rolling averages. First, the unit was never operated at one set of conditions for that long a period during the test program. Also, due to the operating characteristics of the peaking boilers, only 8 to 9 hours per day typically represent full load, steady state operation. Thus, the S02 removal and lime consumption results represent averages of values measured during steady state unit operation for a portion of a number of successive test days. Lime consumption in Tables 2 and 3 is expressed as a reagent ratio, defined as: Reagent Ratio = Calcium in Fresh Lime Fed to System, Ib-mole SO2 in Inlet Flue Gas, Ib-mole (1) (This definition corresponds to that of the term "stoichiometric ratio" in many other dry FGD papers.) Where possible, each value in Table 2 and 3 is supported by alternate calcula- tions. For example, lime slurry feed rates are compared to lime weight belt readings, essentially a calcium balance on the lime slaker. Also, weigh belt readings have been compared against lime truckload delivery inventories. Flue gas flow rates are checked against slurry feed rates by enthalpy balance calculations. Table 2 shows that S02 removal lev- els of nearly 75 percent and 90 percent ------- were achieved for the low sulfur fuel with substoichiometric amounts of lime. This may be attributable to two factors. First, at 35 percent feed slurry solids in low sulfur operation, very high recycle rates are possible. This is seen in the recycle ratio values in Table 2, defined in this report as: Recycle Ratio = Recycle Material in Atomizer Feed Slurry, Ib/hr Fresh Hydrated Lime [Ca(OH)2], Ib/hr (2) Since a large fraction of the baghouse catch and all of the spray dryer bottom solids are recycled, pilot plant results indicate that high sorbent utilization would be promoted. Additionally, anal- yses of the Sarpy Creek coal ash indi- cate a nominal 30 percent alkaline earth content (CaO, MgO, Na20, and K20), be- lieved to have contributed to S02 re- moval. However, the "available alkalin- ity" in the coal ash was not directly measured. The results in Table 2 also show the range of SO2 removal in the spray dryer (S.D.) and fabric filter (F.F.). S02 re- moval in the fabric filter is calculated relative to the spray dryer inlet S02 con- centration as: S02 Removal F.F. - [SO2 into F.F. - SO2 out of F.F.] [S02 into S.D.] (3) With this definition, spray dryer re- moval and fabric filter removal can be summed directly to yield overall re- moval values. The results show that, at 75 percent overall S02 removal, fabric filter removal contributes little to the overall removal. This occurs because sorbent utilization is very high in the spray dryer itself. For 90 percent re- moval, the fabric filter contribution in- creases somewhat, but in an amount roughly proportional to the increase in overall removal level. Table 3 summarizes the high sulfur coal test results. For the first set of data, corresponding to normal low chloride operation, greater than stoichiometric amounts of fresh lime were required. Several factors probably contributed to this effect. One may be that, because of the increased lime addition rates, the re- cycle ratio was greatly reduced relative to low sulfur values in order to maintain the total solids in the slurry at the de- sired weight percent value. Also, the Illi- nois coal ash (being nonalkaline) con- tributed no alkalinity to the S02 removal reactions. For the first set of high sulfur data, the fabric filter contribution to overall S02 removal appears to be more important than for low sulfur operation. Chloride addition has been reported by others to promote increased sorbent utilization in spray-dryer-based FGD systems. The benefits are thought to re- sult from the deliquescent properties of calcium chloride, which delay complete drying of the droplets in the spray dryer and result in higher residual moisture levels in the fabric filter solids. The sec- ond set of S02 removal data in Table 3 corresponds to the addition of calcium chloride at levels which result in a chlo- ride content of 1 percent in the fabric filter solids collected. This chloride level in the fabric filter solids was recom- mended by the system vendor, Niro At- omizer, as being an optimum value for lime utilization enhancement, based on pilot-scale studies conducted at their Copenhagen, Denmark, test facility. At Riverside, this solids chloride level re- quired a liquid-phase chloride concen- tration of about 7,000 ppm in the atom- izer feed slurry. For the recycle rates at Riverside, fresh makeup of calcium chloride accounted for about half of this liquid-phase content, and the remainder dissolved from the recycle material. The results in Table 3 show that chloride ad- dition significantly reduced the lime reagent ratio requirements to achieve nearly 90 percent removal; the lime re- quirement was reduced by about 25 percent. The S02 removal results for these high chloride tests indicate increased SO2 removal across the fabric filter rela- tive to that for the baseline high sulfur coal test. This indicates that the benefits of high chloride level on residual mois- ture level in the fabric filter have a greater impact on S02 removal than im- pacts within the spray dryer. At Riverside, with chloride levels in the fabric filter solids at 1 percent, resid- ual moisture levels increased from below 1 percent to nearly 2 percent. These moisture levels are still low enough to avoid problems which result from handling wet solids. Also, no buildup of wet solids on the spray dryer walls occurred during testing, and solids collected at the bottom of the spray dryer contained moisture levels below 3 percent. These tests were con- ducted at an 18°F approach to adiabatic saturation at the dryer outlet, just as were all previous tests. Material balance calculations indicate that, for a coal such as the Illinois coal fired in the high sulfur tests at Riverside, a chloride content of around 0.3 percent would provide the chloride levels of this test. This would be an uncharacteristi- cally high chloride level for a typical 3.4 percent sulfur coal. However, based on published bulk prices for calcium chlo- ride, it appears that it would be eco- nomic in this case, disregarding capital cost considerations, to operate at high chloride levels even if virtually all of the chloride must be added as calcium chlo- ride. For a 3.4 percent sulfur coal with a higher chloride content (0.1 percent or better), the economics would likely be improved. Additionally, a makeup water source with a significant chloride con- tent, such as some cooling tower blow- downs, should further improve these economics. High chloride levels could potentially have a negative impact on system cor- rosion rates. Corrosion rate impacts could not be measured in this short- term test. No profound impacts were observed, however. Mass Loading Measurement Results Table 4 presents mass loading results for both the high sulfur and low sulfur coal test periods. The results show that the spray dryer increases the grain load- ing at the fabric filter inlet to 3 to 5 times that of the spray dryer inlet value. The data also show that particulate removal levels remained high throughout the test program. Removal efficiencies across the fabric filter varied from 99.95 to over 99.9 percent. The emission lev- els in Table 4 are expressed as grains per dry standard cubic foot. In all cases, particulate emission rates measured were below the current NSPS level for utility boilers (0.03 lb/106 Btu). Flue Gas SO3 Measurement Results Flue gas S03 concentration was also measured. For the low sulfur coal tests, no measurable S03 levels were de- tected at either the spray dryer inlet or fabric filter outlet. The inability to meausre SO3 at the dryer inlet is appar- ently related to the alkaline nature of the Sarpy Creek coal ash. Measurable levels of SO3 were found during the high sulfur test periods. ------- Table 4. Flue Gas Mass Loading Summary Sampling Location Mass Loading, gr/dscf Low Sulfur Tests High Sulfur Tests Spray Dryer Inlet Spray Dryer Outlet Fabric Filter Outlet 3.2 to 4.1 11.0 to 13.8 0.001 to 0.003a 2.8 to 4.1 14.9 to 17.2 0.001 to 0.008b "Equivalent to 0.002 to 0.007 lb/106 Btu. Equivalent to 0.002 to 0.018 lb/106 Btu. Spray dryer inlet values were measured at 2 to 6 ppm S03. Fabric filter outlet values varied from 0.1 to 0.5 ppm. Based on data from a limited number of days where the spray dryer inlet and fabric filter outlet 863 concentrations were measured simultaneously, re- moval efficiencies of 90 percent or bet- ter across the system were indicated. Solid Waste Characteristics Solid waste characteristics for sam- ples collected during both low sulfur and high sulfur test conditions were evaluated in a laboratory-scale test pro- gram. Characteristics of both untreated and cured solid wastes were measured. The cured solid wastes showed best properties for permeability coefficients and unconfined compressive strength when 30 to nearly 50 percent moisture was added to the dry solids before cur- ing. For the 75 percent removal low sul- fur coal tests and the high sulfur coal baseline 90 percent removal tests, per- meability coefficients for cured samples were in the range of 10~5 to 10~7 cm/ sec, typical of treated FGD sludge. Un- confined compressive strengths for these samples were over 100 psi. For the high sulfur coal chloride addition test, however, the permeability coeffi- cient of the cured wastes was increased to the 10~4 range, and the unconfined compressive strength was reduced to 55 psi. Both changes indicate poorer solid waste characteristics, apparently resulting from high chloride levels. Summary and Conclusions Based on results from the 3-month test program on the NSP Riverside dry FGD system, the following conclusions are presented: • In general, the Riverside system ran quite well. None of the problems an- ticipated for spray dryer systems (e.g., rotary atomizer wheel plug- gage, buildup of wet solids on dryer vessel walls, or wetting of fabric fil- ter bag surfaces during upset condi- tions) were observed. • Some problem areas at Riverside appear to be potential sources of problems on similar dry FGD sys- tems. These include typical prob- lems with mixing and pumping slur- ries with a high solids content, solids handling equipment which requires continual maintenance, and sometimes inadequate atom- izer protection during upset condi- tions. • At sulfur levels up to a nominal 3.4 percent, high S02 removal efficien- cies (nearly 90 percent) were readily achievable in the relatively short- term periods of this program. For the low sulfur Sarpy Creek coal/ coke mixutre, substoichiometric amounts of lime were required even at 90 percent S02 removal. This was attributed to the alkaline nature of the Sarpy Creek coal ash. For the high sulfur Illinois coal, 90 percent S02 removal required reagent ratios of about 1.3 to 1.4 moles limes per mole of inlet SO2. • Calcium chloride addition to the at- omizer feed slurry to achieve chlo- ride levels of about 1 percent in the fabric filter solids catch appeared to be successful in promoting lime uti- lization. For the high sulfur tests, the lime reagent ratio to achieve 90 per- cent S02 removal was reduced from 1.3 to 1.4 down to a range of 0.9 to 1.1 moles lime per mole of inlet S02. This chloride level would corre- spond to 0.3 percent chloride in a nominal 3.4 percent sulfur coal. Even for a low chloride, high sulfur coal, high chloride levels achieved through calcium chloride addition appear to be cost effective for re- ducing lime consumption. • Particulate control efficiencies were high throughout the test program, maintaining outlet grain loadings well below required levels. In spite of baghouse operation within 18°F of the adiabatic saturation tempera- ture and very high baghouse inlet grain loadings, no bag-fabric- related problems were observed and flange-to-flange pressure drop remained acceptably low. • For the high sulfur test periods, a limited number of data indicated SO3 removal levels of 90 percent or greater. • Solid waste characteristics for both the low sulfur 75 percent S02 re- moval test and the high sulfur base- line 90 percent S02 removal test ap- pear to be acceptable for landfilling. A deterioration of solid waste char- acteristics was noted, however, for the high sulfur chloride addition tests. Metric Equivalents Nonmetric units are used, for the most part, in this Summary because of their customary usage in the electric power industry. Readers more familiar with their metric counterparts may use the following equivalents: Yields Nonmetric Multiplied by Metric Btu °F ft ft2 ft3 gal. gr hp in2 Ib 1.06 5/9(°F-32) 30.48 0.093 28.3 3.79 0.065 746 6.45 0.45 kJ °C cm m2 L L g w cm2 kg U. 3. GOVERNMENT PRINTING OFFICE: 1985/559-111/20637 ------- G. Blythe, J. Burke, D. Lewis, and C. Thompson are with Radian Corporation, Austin, TX 78758. Theodore G. Brna is the EPA Project Officer (see below). The complete report, entitled "Field Evaluation of a Utility Dry Scrubbing System," (Order No. PB 85-207 488/AS; Cost: $26.50, subject to change) will be available only from: National Technical Information Service 5285 Port Royal Road Springfield, VA22161 Telephone: 703-487-4650 The EPA Project Officer can be contacted at: Air and Energy Engineering Research Laboratory U.S. Environmental Protection Agency Research Triangle Park, NC 27711 United States Environmental Protection Agency Center for Environmental Research Information Cincinnati OH 45268 Official Business Penalty for Private Use $300 EPA/600/S7-85/020 U S ENVIR PROTECTION AGENCY SiSTDhiiSK'lT CHICAGO IL ------- |