United States
 Environmental Protection
 Agency
 Air and Energy Engineering
 Research Laboratory
 Research Triangle Park NC 27711
 Research and Development
 EPA/600/S7-85/020 Aug. 1985
 Project Summary
 Field   Evaluation  of  a  Utility
 Dry  Scrubbing  System

 Gary M. Blythe, Jack M. Burke, David L Lewis, and Carol May Thompson
  This program was the first indepen-
 dent evaluation of a full-scale utility
 spray-dryer/baghouse  dry flue gas
 desulfurization (FGD) system. The eval-
 uated system treats flue gas from a
 nominal 100 MW of coal-fired power
 generation.
  For the test program, two different
 coals were used as boiler fuels: one, a
 subbituminous coal and coke  mixture
 with a nominal 1.2 percent sulfur con-
 tent; and the other, a 3.4 percent sulfur
 Illinois bituminous coal.
  The test program was  conducted
 from July to October  1983. SO2 re-
 moval, participate emissions,  sulfuric
 acid removal, and extensive process
 data were recorded. Low  sulfur coal
 tests indicated that 75 percent SO2 re-
 moval was achievable in the short term
 at reagent ratios of 0.6 to  0.7, and 90
 percent SO2 removal was achievable at
 a reagent ratio of about 0.8.  An average
 removal of  nearly 90 percent was
 achieved in short-term tests with high
 sulfur coal at reagent ratios of 1.3 to 1.4.
 Calcium chloride addition to the atom-
 izer feed slurry was found to reduce the
 lime addition requirements for high sul-
 fur tests by about 25 percent.
  This  Project Summary was devel-
 oped by EPA's Air and Energy Engineer-
 ing Research Laboratory, Research Tri-
 angle Pack, NC, to announce key
 findings of the research project that is
 fully documented in a separate report
 of the same title (see Project Report or-
 dering information at back).

Introduction
  This Summary discusses results from
a program, the objective of which has
been to acquire performance data on an
operating,  utility-scale,  spray-dryer-
based, dry FGD system. The system was
evaluated primarily to determine SO-z
and particulate removal performance
and lime reagent consumption. The sys-
tem chosen for evaluation is the Joy/
Niro Demonstration Unit, at the North-
ern States Power Company (NSP) River-
side Station in Minneapolis, MN. The
Riverside system  was chosen  for this
program because it is the first lime-
based system in operation using a full-
size (46-ft* diameter) spray dryer mod-
ule. Testing was conducted with both
low and high  sulfur boiler fuels. The
program was conducted for the Envi-
ronmental Protection Agency's Air and
Energy Engineering Research  Labora-
tory and for the Electric Power Research
Institute under a  cooperative funding
arrangement.

Project Description
  The project description includes that
of the Riverside station and FGD sys-
tem, a summary of the test program,
and a discussion of the limitations of the
Riverside system and how they have af-
fected this evaluation.

Site Description
  The Riverside generating station, op-
erated by Northern States Power Com-
pany,  in northeast Minneapolis. The
two units of interest on this project,
No. 6  and No. 7,  began operation  in
1949. The combined generating power
of Units 6 and 7 is rated at 98 MW. How-
ever, the pulverized coal, wall-fired
units were originally designed to fire an
eastern bituminous coal. Recently, the
units have fired a western (Sarpy Creek)
subbituminous coal. A  small amount
(10 to 15 percent) of high sulfur coke is
 Readers more familiar with metric units may use
 the conversion table at the back of this Summary.

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   Flue Gas —
   From Unit 7
 Flue Gas
 From Unit 6
                             U Spiral   Grits
                             Claesifter
                                                                                                            Unit 7
                                                                                                            Stack
                                                                                                     ID Fan
                                                                                                            Unit 6
                                                                                                            Stack
                                                                                                     ID Fan
   Slaking
    Water
                         Lime
                         Slurry
                        Storage
                         Trough
                       Atomizer
                       Feed Tank
Figure  1.   Flow diagram for Riverside dry FGD system.
added to the subbituminous coal to im-
prove its firing properties. The units can
still be fired with high sulfur bituminous
coal, and in  fact were so fueled for
5 weeks of this test program.
  In 1980, a full-scale, Joy/Niro, spray-
dryer/fabric-filter FGD system was in-
stalled  to  treat  the combined flue gas
from the two units. The fabric filter was
actually purchased by NSP because of
limitations on the ability of existing ESP
collectors  to efficiently collect the ash
from the western coal. The spray dryer
system was installed  by Joy/Niro under
a cooperative agreement with the utility
to serve as a full-scale demonstration of
the capabilities of their dry FGD system.
Figure 1 is a simplified flow diagram of
the system.
  The spray dryer is  46 ft in diameter,
with flue gas introduced both above the
atomized spray in a roof  gas disperser
and below the atomized spray in a cen:
tral gas disperser. A  rotary atomizer is
used, employing a 700 hp drive motor.
The spray dryer was sized to treat flue
gas corresponding to a  70 MW boiler
load. This reduced sizing permitted sys-
tem tests at greater than design flow
rates. Note that, because Units 6 and 7
are over 30 years  old, the flue gas flow
rate at 70 MW is equivalent to the flue
gas rate from about a 100 MW new unit.
A new unit would  experience much less
air inleakage and operate at  a much
lower net plant heat rate than these
units. The downstream fabric filter con-
tains 12 compartments,  in 2 rows of 6
compartments each. Because the fabric
filter was sized to  treat hot flue  gas, it is
actually oversized when the spray dryer
is in  operation because  of the  flue gas
volume shrinkage which results from
the reduced spray dryer outlet tempera-
ture.
  Pebble lime reagent is slaked  in a Joy/
Denver attrition  slaker.  A Joy/Denver
ball mill is also available for lime slak-
ing. Milk of lime, dilution water, and re-
cycle solids are added to a mix tank at
rates determined by a Honeywell pro-
cess control computer. The mix tank ef-
fluent is pumped to a separate atomizer
feed tank. From the atomizer feed tank,
slurry is pumped to a head tank at the
top of the spray dryer. A pinch-type con-
trol valve regulates the flow of slurry to
the atomizer to maintain either a con-
stant spray dryer outlet temperature or
a constant approach to adiabatic satura-
tion. When the system  is operated to
control  S02 removal, the Honeywell
process control computer calculates the
amount of lime  which must be added
upstream at the mix tank to achieve the
desired  S02 removal. Recycle  material
is added at the  mix  tank at a rate  re-
quired to bring the mix tank solids level
up to a set point, normally 35 weight
percent solids. The  recycle solids are
collected from the spray dryer bottom
dropout and largely supplemented by a

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 portion of the fabric filter catch.

 Testing Approach
   As described in the introduction, a pri-
 mary objective  of the program was  to
 quantify  SO2 removal by the system. A
 continuous  emission  monitoring  sys-
 tem (CEMS) was temporarily installed
 to quantify S02 removal. The CEMS  in-
 cluded a DuPont Model 460 two-point
 extractive S02 monitor and a Thermox
 02  monitor  (sampling the spray dryer
 inlet  and outlet  ducts),  and a Lear
 Siegler SM810 in-situ  point-type  S02
 analyzer  (installed in a short run of duct
 at the fabric filter outlet). A second Ther-
 mox 02 analyzer was mounted on the
 duct exactly opposite the  Lear Siegler
 monitor.
   Other than SO2  removal data, lime
 consumption and  other important  pro-
 cess  parameters  were recorded  as
 hourly averages for each test day. Lime
 consumption was  measured primarily
 by determining the lime content of the
 milk of lime  slurry introduced to the at-
 omizer feed  mix tank. The flow rate  of
 this slurry was  continuously measured
 with a magnetic  flow meter and  re-
 corded by the Honeywell process con-
 trol system computer. Other methods of
 lime consumption  measurement have
 included  continuous quicklime weigh
 belt rate measurements, recording  of
 daily quicklime trucklbad deliveries, and
 determination of the lime  content and
 flow rate of the actual atomizer feed
 slurry. Enthalpy balances have been
 used  to  confirm agreement between
 slurry feed rate and flue gas flow mea-
 surements.
   In addition to quantifying S02  re-
 moval and lime consumption perfor-
 mance for the  spray-dryer/baghouse
 system, determination of particulate re-
 moval performance for  the system was
 also an objective. This performance was
 determined by manual sampling of flue
 gas streams for particulate concentra-
 tions, using  EPA methods. Particulate
 loadings  were measured  at  the spray
 dryer inlet, spray dryer outlet, and fabric
 filter outlet.

 Test Plan
   The test schedule is  summarized  in
 Table  1. These tests were conducted be-
 tween July 11 and October 8, 1983. The
 schedule shows three sets of conditions
 with low  sulfur, Sarpy Creek coal/coke
 blend, and two sets with  high sulfur
 Peabody  Illinois coal. The Sarpy Creek
^coal/coke blend has a  nominal sulfur
"content of 1.1 to 1.2 percent and a heat-
 Table 1.   Test Schedule and Desired System Operation Conditions"
Fuel
Sarpy Creek Coal/Coke
Sarpy Creek Coal/Coke
Sarpy Creek Coal/Coke
Illinois Coal
Illinois Coalb
SO2
Removal
Level,
%
75
75
90
90
90
Fabric
Filter
A/C Ratio,
cfm/ft2
2:1
2.3:1
2:1
2:1
2:1
 "All tests planned to be conducted at at 18°F approach to adiabatic saturation, 35 weight
 percent solids in the atomizer feed slurry, a 70 MW daytime boiler load, a once-per-hour
 baghouse cleaning frequency, and an attrition-type slaker.
 bCalcium chloride addition tests.
 ing value of 9000 Btu/lb.  New Source
 Performance Standards for utility boil-
 ers would require 75 to 80 percent SO2
 removal for boilers firing a fuel with this
 sulfur and heating value. In some locali-
 ties, state or local regulations might re-
 quire as high as 90 percent S02 removal
 with this fuel. Consequently, low sulfur
 tests were conducted at both 75 and 90
 percent target S02 removal levels. Addi-
 tionally, some tests were conducted at a
 fabric filter air-to-cloth ratio higher than
 the nominal value of 2:1.
  Two sets of conditions were tested
 with the high sulfur coal. The coal was
 an Illinois No. 6 coal with a nominal 3.4
 percent sulfur content and 10,700 Btu/lb
 heating value. Current New Source Per-
 formance Standards for utility boilers
 require approximately 90 percent S02
 removal when coal of this sulfur content
 and  heating value  is burned. Conse-
 quently, only a 90 percent target S02
 removal was tested with this high sulfur
 coal. The tests included baseline condi-
 tions  of  90  percent  removal  with
 attrition-slaked lime and a second test
 run employing  calcium  chloride  addi-
 tion for lime utilization  enhancement.
 Chloride addition to enhance lime uti-
 lization in  spray-dryer/baghouse  FGD
 systems has been tested previously in
 bench- and pilot-scale systems, but this
 is the first test of chloride addition at a
full-scale  utility installation. The en-
 hancement effect is thought to occur be-
cause of the deliquescent properties of
calcium chloride.
 System Limitations
  Several system limitations combined
to restrict the amount and the  type of
data that could be collected. First, as
mentioned earlier, Riverside Units 6 and
7 are peaking units. As such, they are
 rarely operated in the winter and only
 operate part-time during July to Octo-
 ber. This  part-time operation involves
 unit loads of 70 to 90 MW during week-
 day daylight hours, minimum load (30
 to 50 MW) overnight during the week,
 and banking the boilers over the week-
 end. Although the FGD system was op-
 erated at desired S02 removal levels 24
 hours per day, only about 12 hours per
 weekday  of near  full-load  operation
 were available for evaluating FGD sys-
 tem performance. At the beginning of
 each 12-hour full-load period, the FGD
 system generally goes through  a tran-
 sient period due to a large increase in
 boiler load. On Mondays, the unit must
 undergo a cold start-up. Although this
 cycling provides a severe test of the ca-
 pabilities of the system, it reduces the
 period of steady state operation at the
 desired S02 removal level over which
 lime reagent consumption can be mea-
 sured.
  Additionally, the Riverside system
 was the first utility-scale system  de-
 signed  and built by Joy/Niro as a
 demonstration unit. As the first unit
 built, the Riverside system has provided
 the opportunity to refine and modify de-
 sign features for subsequent systems.
 Thus, some specifics of the Riverside
 system are different from what  will be
 found in later designs. An example of
 this is the slurry feed system, which has
 been modified for subsequent systems
 to provide quicker response to tran-
 sients such as load changes. At River-
 side, the slurry feed system has  a  resi-
 dence time  of about  1.5 hours. This
 means that following an abrupt process
change, such as a load change,  it  may
take 3 to 4 hours for the slurry feed sys-
tem to stabilize near steady-state condi-
tions.

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  The impacts of the slurry feed prepa-
ration system residence time are partic-
ularly important at the Riverside station,
as the normal station operation causes
significant load  changes at least twice
per day. In fact, on some days during
this test program, the unit load varied
between 70 MW and 90 MW throughout
the day. On these days, the unit never
operated at one load  long enough for
the feed system to stabilize. On most
other days, even if the load was steady
all day, only 8 or 9 hours of the 12 hours
of full load operation actually repre-
sented steady-state conditions.
  Other aspects of the Riverside sys-
tem's status as a demonstration unit af-
fected the results of this program. For
example, the system contains only one
spray dryer module, while most utility
systems will have multiple modules. In
a multiple-module  system, equipment
problems  which affect one individual
module have a smaller impact on over-
all system  performance. Being a one-
module system, equipment problems
tended to  cause the  entire system to
have to be shut down, or operated at
conditions other than those  desired.
Also, because the Riverside system is a
demonstration,  rather than a commer-
cial system, some individual compo-
nents of the system have not  been in-
stalled with the redundancy  that the
vendor would likely install in a commer-
cial system. These considerations have
had a detrimental  effect on both the
amount of system  downtime  and the
number of process-equipment-related
upsets during the test program.
  A final consideration which has af-
fectd the test program involves the re-
cent history of the Riverside station. For
nearly the first 2 years of operation, the
FGD system was used as a full-scale
demonstration and testing unit by the
process vendors. During this time, Joy/
Nirohad responsibility for the operation
of the system, even though NSP actu-
ally provided operating personnel.
Within the  year prior to the test pro-
gram, NSP had assumed responsibility
for the operation of the FGD system. Im-
mediately prior to the test program, the
Units  6 and 7 boilers and FGD system
were off-line for  much of the winter and
spring, as NSP  does not need power
production from these units during this
time. During this long period of down-
time,  normal  personnel turnover (pro-
motions, retirement, transfers, etc.) re-
sulted in a number of new operators
rotating into the FGD  system operating
staff. At the start of the test program,
then, the FGD system was being oper-
ated for the first time in several months
with a staff of operators  having little
previous experience with the FGD sys-
tem. Early in the program, the operators
tended to revert to conservative higher
spray dryer outlet temperatures during
any minor upset, such as soot blowing
in the boilers. This would move the op-
eration away from the desired condi-
tions and would preclude acquiring de-
sired steady state operating data. As the
program  continued, these excursions
occurred  much  less frequently as the
operators became more comfortable
with operating at test conditions.
  Considering the previous discus-
sions, it was not realistic to report avail-
ability of the system, as the availability
of the Riverside system would tell little
about that of a commercial utility, multi-
module, dry FGD system on a new base-
loaded boiler. The combined effects of
weekly cold start-ups, frequent load
changes, little redundance, and a some-
what  undertrained operating staff at
Riverside do little to promote a fair as-
sessment of the potential availability of
a commercial system.
  However, the general operation of the
system was closely observed during the
test program. Much of the downtime or
off-condition operating time was due to
problems specific to the Riverside sys-
tem. Others appear to be more generic
to dry FGD systems. These  more
generic problems are discussed  in the
report, as they are more likely to occur
in other systems.
Results
  The discussion of the program results
is divided into  two areas: Operational
Results, which  includes a qualitative
discussion of the operation  of the
system during  the test  program; and
System Performance, which includes
preliminary S02 removal,  lime con-
sumption, particulate  and sulfuric acid
removal data, and solid waste charac-
teristics.

Operational Results
  In general, the equipment that com-
prises the basis of the dry FGD system,
the spray dryer and baghouse, were rel-
atively trouble-free throughout the pro-
gram. At the conditions tested, the
spray dryer did not show evidence of
potential  problems (e.g., wheel nozzle
pluggage, excessive buildup of solids
on the walls, or formation of wet solids
within the dryer). Some atomizer prob-
lems were observed, but most of these  |
appeared to be caused by  circum-
stances specifc to the situation at River-
side rather than being generic to the
Joy/Niro  system. These  problems will
be discussed further later in this section.
  The  baghouse also operated  well,
with no significant bag/fabric related
problems  being  observed. In this
short-term  test though,  long-term  ef-
fects such as bag life or compartment
wall corrosion rates could not be evalu-
ated.
  Some problems were observed in
four specific areas—the slurry feed sys-
tem, the ash handling  system, the ball
mill slaker, and in atomizer protection.
The system  vendors may have ad-
dressed these problems  in system de-
signs subsequent to Riverside, but the
problems could be  encountered in vir-
tually any spray-dryer-based  dry FGD
system. Each of these areas is discussed
below.

Slurry Feed System
  In a recycle lime system, lime slurries
containing up to 25 percent solids and
recycle/lime slurries of 30 to 40 percent
solids  are commonly encountered.
When dealing with  slurries with a high
solids content and high viscosity, prob-
lems (e.g.,  plugging of pump suction
lines, solids buildup on tank walls, plug-
ging of in-line screens used to remove
oversize material, and loss of flow when
switching pumps)  are commonly en-
countered. Such problems were en-
countered often at the Riverside sys-
tem. Years of operation  of wet  lime/
limestone FGD systems have estab-
lished means of dealing with such prob-
lems. The quantities  of  these slurries
that must be dealt with in a spray  dryer
system, though, are much smaller than
what would be encountered  in  a wet
system. At Riverside,  typical  atomizer
feed slurry rates are 150 to 200 gpm. In
a similarly sized limestone wet  FGD sys-
tem, the slurry recirculation rate could
be as high as 40,000 gpm. While some
of the slurry handling problems of a wet
FGD system may still be encountered in
a spray dryer system, they will  occur on
a greatly reduced  size of equipment.
This should make both problem solving
and  routine maintenance easier. An-
other important point to be noted is that
chemical scaling tendencies were not
observed at Riverside.

Ash Handling System
  In comparing the wet versus dry FGD t
systems, the spray dryer system has a *

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 slurry feed system that deals with much
 lower flow rates for a given unit capac-
 ity, but the  quantities of dry ash and
 FGD by-products that must be moved
 around the  system are substantially
 greater than  for a comparably sized par-
 ticulate collection device/wet  scrubber
 system.
   The  problem with solids handling
 which most frequently occurred at
 Riverside involved the baghouse me-
 chanical conveyors, blow pots, and the
 recycle bin rotary valve. Failures in any
 of these components could interrupt the
 flow of recycle material to the slurry mix
 tank, and cause the system to approach
 once-through operation.

 Ball Mill Slaker
   During this program, the  ball mill
 slaker  did not operate successfully for
 any  extended period: the  feed end of
 the slaker tended to plug with wet lime
 solids. While there  are several possible
 reasons why the plugging continually
 occured, the actual cause was  not iden-
 tified.
   The ball mill slaker problems at River-
 side appear to be  somewhat site-
 specific (ball mill slakers  have operated
 successfully  elsewhere).  In retrospect,
 the slaker might have run more success-
 fully  at a higher water-to-lime ratio, re-
 sulting in a less viscous  product slurry
 and less vapor release. However, in the
 attempts to run the ball mill slaker dur-
 ing the high sulfur tests in particular, the
 slaking water piping size did not allow
 operation at higher water-to-lime ratio
 at the lime slaking  rates  required. Dur-
 ing the high sulfur tests, lime slaking
 rates averaged  approximately four
 times that required for the normal low
 sulfur fuel at similar unit load  and per-
 cent  S02 removal conditions.

 Atomizer Problems
   Although the atomizer motor, gear-
 box,  and nozzle wheel were generally
 trouble-free,  on several occasions prob-
 lems which  could  result in  atomizer
 damage were observed.
   Two  scenarios  for potential  damage
 were observed. One occurred when the
 unit was forced to run from the basic, or
 less sophisticated, control station of the
 computer control  system while the
 more sophisticated  supervisory station
 was  undergoing repair. The control
 software at Riverside does not have full
 interlock protection for  the  atomizer
 when running from the  basic station.
. (Interlocks are software which automat-
ically shut down the  atomizer  when
 Table 2.   SO^ Removal Results, Low Sulfur Coal
Average
SO2
Removal,
%
74
75b
89
Spray
Dryer
Removal,
%
_a
67
78
Fabric
Filter
Removal,
%
_a
8
11
Reagent
Ratio
0.7
0.6
0.8
Recycle
Ratio
13:1
14:1
11:1
 "Not measured.
 Increased air-to-cloth ratio at fabric filter; other tests at normal air-to-cloth ratio.

 Table 3.   S02 Removal Results, High Sulfur Coal
Average
S02
Removal,
%
88
89a
Spray
Dryer
Removal,
%
72
62
Fabric
Filter
Removal,
%
16
27
Reagent
Ratio
1.3
1.0
Recycle
Ratio
2:1
3:1
aHigh chloride concentration tests.

given inputs that are indicators of prob-
lems which might result in damage to
the  atomizer.) While running  in this
mode, a minor problem involving loose
wires  to the  atomizer  oil circulating
pump  occurred, intermittently shutting
off the pump. However, the basic sta-
tion only gave the control operator an
alarm  rather than shutting down the
atomizer automatically. The atomizer
continued  to  run for several minutes
without oil circulation and sustained
gearbox damage.
  The second  scenario which could re-
sult  in  atomizer damage was observed
on more than one occasion: it involved
feeding slurry to the atomizer wheel
when it was not rotating. Since the non-
rotating wheel has  a  much lower hy-
draulic capacity than a rotating  wheel,
slurry fed to the standing wheel tends to
overflow the wheel and can flow up the
spindle to which the wheel is attached
and  enter the atomizer oil system. In
such instances, the oil sump can be im-
mediately emptied and flushed to avoid
damage, but if the atomizer is operated
before cleaning, the slurry in the oil can
eventually cause gearbox damage.

System Performance
  The results of S02 removal and lime
consumption  measurements during
this  test program are summarized in
Tables 2 and 3. Table 2 summarizes the
low  sulfur  coal SO2 removal results;
and Table 3 summarizes those for the
high sulfur  coal tests.
  For several reasons, the SC>2 removal
results from the program cannot be ex-
pressed  as 30-day rolling averages.
First, the unit was never operated at one
set of conditions for that long a period
during the test program. Also, due to
the operating characteristics of the
peaking boilers,  only 8 to  9 hours  per
day typically represent full  load, steady
state operation. Thus, the S02 removal
and lime consumption results represent
averages  of values measured during
steady state unit operation for a portion
of a number of successive test days.
  Lime consumption in Tables 2 and 3 is
expressed as a reagent ratio,  defined
as:

Reagent Ratio =
       Calcium in Fresh Lime
      Fed to System, Ib-mole
   SO2 in Inlet Flue Gas, Ib-mole
(1)
(This definition corresponds to that of
the term "stoichiometric ratio" in many
other dry FGD papers.)
  Where possible, each value in Table 2
and 3 is supported by alternate calcula-
tions. For example, lime slurry feed
rates are compared to lime weight belt
readings, essentially a calcium balance
on the lime slaker. Also, weigh  belt
readings have been compared against
lime truckload delivery inventories. Flue
gas flow rates are checked against
slurry feed  rates  by enthalpy balance
calculations.
  Table 2 shows that S02 removal lev-
els of nearly 75 percent and 90 percent

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were achieved for the low sulfur fuel
with substoichiometric amounts  of
lime. This may be attributable to two
factors.  First, at 35 percent feed slurry
solids in low sulfur operation, very high
recycle  rates are possible. This is  seen
in the recycle ratio  values in Table 2,
defined  in this report as:

Recycle  Ratio =
    Recycle Material in Atomizer
         Feed Slurry, Ib/hr
       Fresh Hydrated Lime
          [Ca(OH)2], Ib/hr
(2)
Since a large fraction of the baghouse
catch and all of the spray dryer bottom
solids are recycled, pilot plant  results
indicate  that high sorbent  utilization
would be promoted. Additionally, anal-
yses of the Sarpy Creek coal ash  indi-
cate a nominal 30 percent alkaline earth
content (CaO, MgO, Na20, and K20), be-
lieved to have contributed to S02 re-
moval. However, the "available alkalin-
ity"  in the coal  ash was not directly
measured.
  The results in Table 2 also show the
range of SO2 removal in the spray dryer
(S.D.) and  fabric filter (F.F.). S02 re-
moval in the fabric filter is  calculated
relative to the spray dryer inlet S02 con-
centration as:
S02 Removal
            F.F. -
   [SO2 into F.F. - SO2 out of F.F.]
          [S02 into S.D.]
(3)
With this definition, spray dryer re-
moval and fabric filter removal can be
summed directly to yield  overall re-
moval values. The results show that, at
75 percent overall S02 removal, fabric
filter removal  contributes little to the
overall removal. This occurs because
sorbent utilization  is very high in the
spray dryer itself. For 90 percent re-
moval, the fabric filter contribution in-
creases somewhat,  but in an  amount
roughly proportional to the increase in
overall removal level.
  Table 3 summarizes the  high sulfur
coal test results. For the first set of data,
corresponding to normal low  chloride
operation,  greater than stoichiometric
amounts of fresh lime were required.
Several factors probably contributed to
this effect. One may be that, because of
the increased lime addition rates, the re-
cycle ratio was greatly reduced relative
to low sulfur values in order to maintain
the total solids in the slurry at the de-
sired weight percent value. Also, the Illi-
nois coal ash (being nonalkaline) con-
tributed no alkalinity to the S02 removal
reactions. For the first set of high  sulfur
data, the fabric filter contribution to
overall S02 removal appears to be more
important than for low sulfur operation.
  Chloride addition has been reported
by others to promote increased sorbent
utilization in spray-dryer-based FGD
systems. The benefits are thought to re-
sult from the deliquescent properties of
calcium chloride, which delay complete
drying of the droplets in the spray dryer
and  result in higher residual moisture
levels in the fabric filter solids. The sec-
ond set of S02 removal data in Table 3
corresponds to the addition of calcium
chloride at levels which result in a chlo-
ride  content of 1  percent in the  fabric
filter solids collected. This chloride level
in the fabric filter solids was recom-
mended by the system vendor, Niro At-
omizer, as being an optimum value for
lime utilization enhancement, based on
pilot-scale studies conducted  at their
Copenhagen, Denmark, test  facility. At
Riverside, this solids chloride level re-
quired a liquid-phase chloride concen-
tration of about 7,000 ppm in the  atom-
izer feed slurry. For the recycle rates at
Riverside,  fresh  makeup of calcium
chloride accounted for about half  of this
liquid-phase content, and the remainder
dissolved from the recycle material. The
results in Table 3 show that chloride ad-
dition  significantly reduced the lime
reagent ratio requirements to achieve
nearly 90 percent removal; the lime re-
quirement  was reduced  by about
25 percent.
  The  S02 removal results for  these
high chloride tests indicate increased
SO2 removal across the fabric filter rela-
tive to that for the baseline high  sulfur
coal test. This indicates that the benefits
of high chloride level on residual mois-
ture level in the fabric  filter have a
greater impact on S02 removal than im-
pacts within the spray dryer.
  At Riverside, with chloride levels in
the fabric filter solids at 1 percent, resid-
ual moisture levels increased from
below 1  percent to  nearly 2 percent.
These moisture levels  are still low
enough to avoid problems which result
from handling wet solids. Also, no
buildup of wet solids on the spray dryer
walls  occurred during  testing, and
solids  collected at the bottom of the
spray dryer contained moisture  levels
below 3 percent. These tests were con-
ducted at an 18°F approach to adiabatic
saturation at the  dryer outlet, just as
were all previous tests.
  Material balance calculations indicate
that, for a coal such as the Illinois coal
fired in the high sulfur tests at Riverside,
a chloride content of around 0.3 percent
would provide the chloride levels of this
test. This would be an uncharacteristi-
cally high chloride level for a typical 3.4
percent sulfur coal. However,  based on
published bulk prices for calcium chlo-
ride, it appears that it would be eco-
nomic in this case, disregarding capital
cost considerations, to operate at high
chloride levels even if virtually all of the
chloride must be added as calcium chlo-
ride. For a 3.4 percent sulfur coal with a
higher chloride content (0.1 percent or
better), the economics would likely be
improved. Additionally, a makeup water
source with a significant chloride con-
tent, such as some cooling tower blow-
downs, should further  improve these
economics.
  High chloride levels could potentially
have a negative impact on system  cor-
rosion rates. Corrosion rate impacts
could not be measured in this short-
term test. No profound  impacts were
observed, however.

Mass Loading Measurement
Results
  Table 4 presents mass loading results
for both the high  sulfur and low sulfur
coal test periods. The results show  that
the spray dryer increases the grain load-
ing at the fabric filter inlet to 3 to 5 times
that of the spray dryer inlet value.  The
data also show that particulate removal
levels  remained high  throughout the
test program. Removal efficiencies
across the fabric filter varied from 99.95
to over 99.9 percent. The emission lev-
els in Table 4 are expressed  as grains
per dry standard cubic foot. In all cases,
particulate emission rates measured
were below the current NSPS level for
utility boilers (0.03 lb/106 Btu).

Flue Gas SO3 Measurement
Results
  Flue gas S03 concentration was  also
measured. For the low sulfur coal tests,
no measurable S03 levels  were de-
tected at either the spray dryer inlet or
fabric filter  outlet. The inability to
meausre SO3 at the dryer inlet is appar-
ently related to the alkaline nature of the
Sarpy Creek coal ash.
  Measurable levels of SO3 were found
during the  high  sulfur test periods.

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 Table 4.   Flue Gas Mass Loading Summary
    Sampling
     Location
                                             Mass Loading, gr/dscf
Low Sulfur Tests
High Sulfur Tests
 Spray Dryer Inlet

 Spray Dryer Outlet

 Fabric Filter Outlet
   3.2 to 4.1

  11.0 to 13.8
 0.001 to 0.003a
                                                                 2.8 to 4.1
   14.9 to 17.2

 0.001 to 0.008b
 "Equivalent to 0.002 to 0.007 lb/106 Btu.
 Equivalent to 0.002 to 0.018 lb/106 Btu.

 Spray dryer inlet values were measured
 at 2 to  6 ppm  S03. Fabric filter outlet
 values  varied  from 0.1 to 0.5 ppm.
 Based on data from a limited number of
 days where the spray dryer  inlet and
 fabric filter  outlet 863 concentrations
 were measured simultaneously,  re-
 moval efficiencies of 90 percent or bet-
 ter across the system were indicated.

 Solid Waste Characteristics
  Solid  waste characteristics  for sam-
 ples collected during  both low sulfur
 and  high sulfur test conditions were
 evaluated in a laboratory-scale test pro-
 gram. Characteristics of both untreated
 and cured solid wastes were measured.
 The  cured solid wastes  showed best
 properties for permeability coefficients
 and  unconfined compressive strength
 when 30 to nearly 50 percent moisture
 was  added to the dry solids before cur-
 ing. For the 75 percent removal low sul-
 fur coal tests and the  high sulfur coal
 baseline 90 percent removal tests, per-
 meability coefficients for cured samples
 were in the  range of 10~5 to  10~7 cm/
 sec,  typical of treated FGD sludge. Un-
 confined compressive strengths for
 these samples were over 100 psi.  For
 the high sulfur coal chloride addition
 test, however, the permeability coeffi-
 cient of the cured wastes was increased
 to the 10~4 range, and the unconfined
 compressive strength was reduced  to
 55 psi.  Both changes  indicate poorer
 solid  waste  characteristics, apparently
 resulting from high chloride levels.

 Summary and Conclusions
  Based  on  results from the  3-month
test program on the NSP Riverside dry
 FGD  system, the following conclusions
are presented:
  • In general, the Riverside system ran
   quite well. None of the problems an-
   ticipated for spray dryer  systems
   (e.g., rotary atomizer wheel  plug-
   gage, buildup of wet solids on dryer
   vessel walls, or wetting of fabric fil-
   ter bag surfaces during upset condi-
   tions) were observed.
          • Some problem areas at Riverside
           appear to be  potential  sources of
           problems on similar dry FGD sys-
           tems. These include typical  prob-
           lems with mixing and pumping slur-
           ries with a high  solids content,
           solids handling equipment which
           requires continual maintenance,
           and sometimes inadequate atom-
           izer protection during upset condi-
           tions.
          • At sulfur levels up to a nominal 3.4
           percent, high S02 removal efficien-
           cies (nearly 90 percent) were readily
           achievable in  the  relatively short-
           term  periods of this program. For
           the low  sulfur Sarpy Creek coal/
           coke mixutre, substoichiometric
           amounts of lime were required even
           at 90 percent S02 removal. This was
           attributed to the alkaline nature of
           the Sarpy Creek coal ash.  For the
           high sulfur Illinois  coal,  90  percent
           S02 removal required reagent ratios
           of about 1.3  to 1.4  moles limes per
           mole of inlet SO2.
          • Calcium chloride addition to the at-
           omizer feed  slurry  to achieve chlo-
           ride levels of about 1 percent in the
           fabric filter solids catch appeared to
           be successful in promoting lime uti-
           lization. For the high sulfur tests, the
           lime reagent ratio to achieve 90 per-
           cent S02 removal was reduced from
           1.3 to 1.4 down to a range of 0.9 to
           1.1 moles lime per mole of inlet S02.
           This chloride level would corre-
           spond to 0.3 percent chloride in  a
           nominal  3.4 percent sulfur  coal.
           Even for a low chloride, high sulfur
           coal, high chloride levels achieved
           through calcium chloride addition
           appear to be cost  effective for re-
           ducing lime consumption.
         • Particulate control efficiencies were
           high throughout the test program,
           maintaining  outlet grain loadings
           well below required levels. In spite
           of baghouse operation within 18°F
           of the adiabatic saturation tempera-
           ture and  very high baghouse inlet
    grain loadings, no  bag-fabric-
    related  problems were observed
    and flange-to-flange pressure drop
    remained acceptably low.
  • For the  high sulfur test periods, a
    limited  number  of data indicated
    SO3 removal levels of 90 percent or
    greater.
  • Solid waste characteristics for both
    the low  sulfur 75 percent S02 re-
    moval test and the high sulfur base-
    line 90 percent S02 removal test ap-
    pear to be acceptable for landfilling.
    A deterioration of solid waste char-
    acteristics was noted, however, for
    the high sulfur chloride addition
    tests.

Metric Equivalents
  Nonmetric units are  used, for the
most part, in this Summary because of
their  customary usage in the electric
power industry. Readers more familiar
with their metric counterparts may use
the following equivalents:
                              Yields
Nonmetric    Multiplied by    Metric
Btu
°F
ft
ft2
ft3
gal.
gr
hp
in2
Ib
1.06
5/9(°F-32)
30.48
0.093
28.3
3.79
0.065
746
6.45
0.45
kJ
°C
cm
m2
L
L
g
w
cm2
kg
                                                                              U. 3. GOVERNMENT PRINTING OFFICE: 1985/559-111/20637

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   G. Blythe, J. Burke, D. Lewis, and C.  Thompson are with Radian Corporation,
     Austin, TX 78758.
   Theodore G. Brna is the EPA Project Officer (see below).
   The complete report, entitled "Field Evaluation of a Utility Dry Scrubbing System,"
     (Order No.  PB 85-207 488/AS;  Cost: $26.50, subject to change) will be
     available only from:
          National Technical Information Service
          5285 Port Royal Road
          Springfield, VA22161
          Telephone: 703-487-4650
   The EPA Project Officer can be contacted at:
          Air and Energy Engineering Research Laboratory
          U.S. Environmental Protection Agency
          Research Triangle Park, NC 27711
United States
Environmental Protection
Agency
Center for Environmental Research
Information
Cincinnati OH 45268
Official Business
Penalty for Private Use $300
EPA/600/S7-85/020
       U  S  ENVIR  PROTECTION  AGENCY
       SiSTDhiiSK'lT
       CHICAGO               IL

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