United States
Environmental Protection
Agency
Municipal Environmental Research
Laboratory
Cincinnati OH 45268
Research and Development
EPA-600/S2-83-105  Feb. 1984
Project  Summary
Sewage  Sludge  Incinerator  Fuel
Reduction  at  Nashville,
Tennessee
Albert J. Verdouw and Eugene W. Waltz
  A field demonstration  project was
 conducted to reduce fuel consumption
 in municipal sludge incinerators using a
 more fuel efficient incinerator operating
 mode, which was developed at Indian-
 apolis, Indiana, Belmont Treatment
 Plant. The Nashville-Davidson County
 Department  of Water and Sewerage
 Services demonstrated the new operat-
 ing mode in Nashville, TN, with the use
 of two, conventional,  multiple hearth
 incinerators.
  The more fuel efficient operating
 mode was developed from an extensive
 program  of  combustion  engineering
 measurement, testing, and operational
 analysis.  Incinerator operators were
 given on-the-job training in  the new
 operating mode during a 30-day dem-
 onstration-training period. After 1 year
 of routine operations in the new mode,
 the use of fuel was reduced more than
 40%; this represents fuel cost savings
 of approximately $.350,000 per year.
  The project exemplified how cost
 effective efforts  can improve and
 optimize existing incinerator operation.
 This project also successfully transferred
 and applied incinerator operating tech-
 nology developed by the City of Indian-
 apolis Department of Public Works and
 the Indianapolis Center for Advanced
 Research under sponsorship of the U.S.
 EPA Municipal Environmental Research
 Laboratory.  The Indianapolis work
 included a projection that most plants
 could reduce their fuel costs 20% to
 50% if fuel  efficient  operation were
 used, and this work confirms that
 projection.
  This Project Summary was developed
 by EPA's Municipal Environmental
Research Laboratory.  Cincinnati, OH,
to announce key findings of the research
project that is fully documented in a
separate report of the same title (see
Project Report ordering information at
back).

Introduction
  Because incinerating municipal sewage
sludge  often  uses large  amounts  of
auxiliary fuel,  increasing energy costs
have made incinerator fuel consumption
a major operating problem. Using more
fuel efficient operating modes can reduce
this consumption, and efforts to optimize
existing operating systems can be cost
effective for municipal operators.
  The Department of Water and Sewerage
Services of Nashville-Davidson  County
designed  a  new,  more fuel efficient
operating  mode by adapting incinerator
operating technology developed in Indi-
anapolis, IN.  The Nashville Center
Wastewater Treatment Plant has two 10-
hearth incinerators with a design capacity
of 10 wet tons of sludge cake per
incinerator per hour.  With technical
assistance from the Indianapolis Center
for  Advanced Research, the Nashville-
Sewerage Department conducted  a
series of operational tests, measurements,
and analyses to determine the specific
operating settings  and improvements
required to reduce fuel consumption and
achieve steady incinerator  operation. A
combustion engineering analyses was
made of the complete incinerator opera-
tion including measurements of specific
air flow rates,  fuel flow, and load rate
dependent performance  parameters.
  Performance tests determined the fuel
consumption performance of the rnciner-

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ators at specific settings for excess air,
load rate, sludge  cake moisture and
volatile characteristics, total  airflow,
burner use profile, and various airflow
management  approaches  suited to the
given  equipment design and operational
set-up.
  A kinetic incinerator analytical model
was also used to predict the lowest fuel
consumption  possible with optimum
incinerator operation The  model's pre-
dictions of incinerator fuel requirements
provided  a  process-rate-determined
solution accounting for gas temperatures.
sludge composition,  and  heat transfer
rates, which vary throughout the inciner-
ator volume.
  These test results were then used  to
specify a  new,  more fuel   efficient
operating mode for trial testing  and
demonstration.

New  Operating Mode
  In the past, incinerator operation was
characterized by each  operator having
his own specific operating practices and
techniques for maintaining temperatures
on various hearth levels and for managing
incinerator airflow.  Several   common
operating problems were associated with
the operator-specific modes:
  • incinerator exhaust temperatures
    were too high  in the furnace,
  • incinerator draft pressure was
    greater than necessary,
  • rabble arm cooling air return was
    underutilized,
  • auxiliary air  supply was  being
    overused, and
  • burner use  pattern were  not opti-
    mum.
Other problem  areas, including  the
management of the sludge cake loading
to the incinerators, were also contributing
to high fuel consumption.
  The  new  operating  mode  included
specific, detailed settings  for optimizing
the combustion zone location, airflow
management, fuel flow rates needed for
given  sludge  cake  load ranges, and
moisture and volatile characteristics. The
key features  of the operating mode
involved operational settings to maintain:
  • a steady sludge cake feed  rate,
  • the lowest possible incinerator draft
    to reduce air leakage,
  • the proper oxygen level  associated
    with a given load rate to  maintain
    the most efficient excess air level,
  • the minimum required fuel flow rate
    for a given load,
  • control of combustion zone location
    with burner use firing profiles and
    air flow management, and
  • optimum throughput rate with
    proper center shaft drive speed.

Results
  A full, plant scale, operational demon-
stration test was conducted to determine
how  much fuel was saved by using a
more fuel  efficient operating mode. The
10-month  operational test  period  was
from November  1980 through August
1981. A 29-month baseline operational
period was used for comparison (January
1, 1978, through May 31, 1980). Plant
operational recoids for both periods were
used to obtain fuel consumption,  load
rates, incinerator  operating hours, and
sludge cake moisture and volatile data for
comparative analyses. The principal
measure  used for comparing fuel con-
sumption was specific fuel consumption
(SFC) defined in cubic feet of gas per dry
ton of sludge cake incinerated. The SFC is
also directly related to the absolute ratio
of the  sludge cake  moisture to volatile
content (M/V) on a weight basis.  An ac-
curate  comparison of SFC must account
and  correct for the M/V ratio  of the
sludge cake being incinerated to avoid a
distorted comparison. For this reason, the
relationship of the daily average SFC with
the sludge cake M/V ratio was computed
and compared for the two periods.
  A  least squares  regression analysis
was made for the SFC versus sludge cake
M/V ratios  for both time periods. The
results of these analyses can be compared
in Figure 1. Table 1 shows the respective
averages of the other operational variable
for the two time periods.
  As shown in Figure  1, the SFC was
reduced, as well as the basic relationship
between SFC and the sludge cake M/V
ratio, reflected by the decreased  rate of
increase of SFC with M/V ratio.  At the
low M/V  ratio of 6, the computed SFC
difference was 22.6%,  and at the high
M/V ratio of 10, the difference was 42%.
For the 10-month period, the average fuel
reduction was 38.9%.
  The 38.9% reduction represented a fuel
savings of 5,612 cubic feet of gas  per dry
ton of cake incinerated. For the 10-month
period, the total  fuel  savings  was
59,670,154 cubic  feet of gas. At this
reduction  level, the annual gas savings
was approximately 71,604,180 cubic feet
of gas that, at a gas price of $3.50 per
1000  cubic feet,  represents  direct
savings of $250,000 per year for incin-
eration fuel.
  Operational records were also analyzed
to determine the reduction in standby fuel
resulting  from  improved  sludge load
management to the two incinerators as
part of the new operating procedures. The
plant  loading rate was not large enough
to keep both incinerators on line at, or
near,  design capacity. The past practice
had  been to run  both incinerators at
capacity until the sludge inventory level
was reduced to a point that one of the
incinerators  had to be put on  standby
operation. In the new operating mode,
both incinerators were operated contin-
uously at  lower  loading  rates thus
enabling the standby fuel use to be
drastically  reduced. Comparison of
standby fuel use rates during  the 10-
month demonstration period with past
operational averages showed a dramatic
75% reduction amounting to 2,300,000
cubic feet of gas per month—an annual
savings of $96,000 per year.
  The total  combined incineration and
standby fuel savings by the  Nashville
operations using the new operating mode
was approximately $350,000 per year.

Conclusions
  The principal conclusions from this in-
plant research and demonstration project
were that:
   • incinerator auxiliary fuel consump-
     tion can be significantly reduced by
     using more fuel efficient operating
     modes  derived from new operating
     technology and experience;
   • fuel reductions can be easily and
     quickly  achieved through operational
     changes alone in existing facilities
     without having to make  major  or
     high cost equipment changes;
   • multiple hearth  sludge incinerator
     technology  can be cost effectively
     transferred  and applied to many
     municipal operations because of the
     similarity in  equipment operational
     practices;
   • a 40%  fuel reduction was achieved
     over a 10-month demonstration per-
     iod representing an  annual  cost
     savings of approximately $350,000
     per year;
   • this work serves to substantiate the
     analysis made for the Indianapolis
     work, which indicated that savings
     of 20% to 50%  are possible if the
     plants  are  operated  in the fuel
     efficient mode.            ^

   The full  report was  submitted  in
fulfillment of Contract No. 68-02-3487 by
Battelle Columbus Laboratories under
the sponsorship of the U.S. Environmental
Protection Agency.

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                            10 Month Average Reduction
                                                                         42.3%
22.6%
Figure  1.
      6789

           Sludge Cake Moisture to Volatile Ratio IM/V) ftb/lb)

Specific fuel consumption comparison.
                                                                        10
Table 1.    Average Daily Values of Key Operating Variables for Baseline anil Demonstration
Variable
Wet Tons
Dry Tons
Percent Solids
Percent Volatiles*
M/V Ratio
SFC (1000 ft /dry ton)
* % Volatiles - thermally
(% volatiles
Baseline Demonstration
Period Period
129 Months) (10 Months)
202
35.7
17.8
61.9
7.7
144
volatile portion of the dry solids
+ % ash - 100% dry sludge)
226
358
161
62.9
8.7
8.8

Percent
Difference
*24
+ 1
- 1.7
* 10
+ 1.0
- 56

  Albert J. Verdouw and Eugene W.  Waltz are with the Indianapolis Center for
    Advanced Research, Indianapolis.  IN 46204.
  Howard O. Wall is the EPA Project Officer (see below).
  The complete report, entitled "Sewage Sludge Incinerator Fuel Reduction at
    Nashville. Tennessee," (Order No. PB 84-113 075; Cost: $10.00, subject to
    change) will be available only from:
          National Technical Information Service
          5285 Port Royal Road
          Springfield, VA22161
          Telephone: 703-487-4650
  The EPA Project Officer can be contacted at:
          Municipal Environmental Research Laboratory
          U.S. Environmental Protection Agency
          Cincinnati, OH 45268
ftUS. GOVERNMENT PRINTING OFFICE 1984-759-015/7297

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United States                         Center for Environmental Research
Environmental Protection               Information
Agency                               Cincinnati OH 45268
Official Business
Penalty for Private Use $300
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