United States
                    Environmental Protection
                    Agency
Air and Energy Engineering
Research Laboratory
Research Triangle Park NC 27711
                    Research and Development
 EPA/600/S2-85/139  Jan. 1986
&EPA         Project Summary
                    Hyperfiltration  for  Textile
                    Preparation  Caustic  Discharge
                    Reduction
                    Craig A. Brandon
                      Hyperfiltration (HF)  is a membrane
                    separation technique  widely used in
                    desalination of natural water and in
                    some industrial separation applications.
                    Because energy, process chemicals, and
                    water are discharged  from  industrial
                    processes in large quantities, recycle
                    has been studied with the objectives of
                    energy and material conservation and
                    pollution  abatement.  The  results  of
                    several research projects with formed-
                    in-place membranes are the background
                    for the current project,  which is the
                    joining of an HF system with an oper-
                    ating caustic scour and preparation
                    range in an integrated textile dye and
                    finishing plant. The effluent treated by
                    HF is a 3 to 10 weight percent caustic
                    (NaOH) solution. The caustic percent-
                    age  and  the amounts and  types  of
                    contaminants in the effluent depend on
                    the style  and weight  of fabric being
                    processed.
                      HF  membranes formed on porous
                    sintered-steel tubular supports are used
                    to remove contaminants from a hot
                    (95°C) caustic scour solution and render
                    it reusable for scouring. For this demon-
                    stration over 15 million m of approxi-
                    mately 1.5 m wide fabric was scoured
                    using over 3 million L of recycled caustic
                    solution. The initial prototype unit was
                    replaced with an improved design, using
                    316L stainless steel porous material to
                    achieve the necessary corrosion resist-
                    ance.
                      Results of this prototype project indi-
                    cated a positive  rate  of return  with
                    savings estimated at  $379,900/yr,
                    greatly exceeding the installed capital
                    ($361,500) and  operating ($37.9007
                    yr) costs. The prototype unit is being
expanded from 100 to 210 m2, and a
second 220 m2 HF unit is also being
installed.
  The report describes the applicable
textile process, the reuse scenario, and
the HF unit and its operation.

  This Project Summary was developed
by EPA's Air and Energy Engineering
Research Laboratory. Research Triangle
Park, NC. to announce key findings of
the research project that is fully docu-
mented in a separate report of the same
title (see Project Report ordering infor-
mation at back).

Introduction
  The technical feasibility of using formed-
in-place hyperfiltration (HF) membranes
to renovate a variety of textile waste-
waters for direct recycle was shown in a
series of research projects conducted as '
part of a cooperative program between
the textile industry and the U.S.  EPA,
beginning in 1972.  The current project
demonstrates the use of an HF unit to
recycle 3 to 10 weight percent caustic
(NaOH) at 95°C from a  cotton scour
saturator. This project was funded by a
cooperative agreement between the EPA
and CARRE, Inc. The Graniteville Com-
pany, Graniteville, SC, provided the cap-
ital equipment and evaluated the produc-
tion procedures used during testing.
  The wide scale implementation of HF to
recycle caustic process effluents would
have a large impact on pollution abate-
ment. The cost of achieving this pollution
abatement with HF would be offset by the
combination of savings from the simul-
taneous recovery of energy and caustic
solution. In  addition, the subsequent

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waste  treatment of the  concentrated
contaminants may be improved because
of the reduced  volume  of  the waste
stream.

Hyperfiltration
  Hyperfiltration  is a fluid  separation
process utilizing a semi-permeable mem-
brane.  Permeation  through  the mem-
brane is driven by pressure differential.
Since the separation is achieved without
a change of phase, membrane separation
is inherently more energy efficient than
processes involving a phase change; e.g.,
evaporation or freezing.  The optimized
single-pass arrangement, which requires
no  recirculation  of any concentrated
material, utilizes  about  10 BtuVkg  of
solvent passing through the membrane,
or about 30 Btu/kg of solvent separated.
Change-of-phasetechnologies(e.g., freez-
ing and evaporation) require 4 to40 times
as much energy per kilogram of solvent
separated.
  Initial interest in membrane separation
was largely directed to desalination of sea
and brackish  water. Attempts to utilize
the technology in industrial  situations
encountered restrictions  due  to the in-
ability  of commercially available equip-
ment  to tolerate the high temperature
and corrosive composition of the typical
industrial waste streams. The innovation
of zirconium oxide/polyacrylic acid
(ZOPA) membranes (formed in place on
sintered stainless steel  tubes) relaxed
many  of the  limitations. ZOPA mem-
branes were utilized in the prototype HF
system studied in this project.

Textile Caustic Recovery
  Caustic  solutions are  used to clean
equipment and products in many indus-
tries. A survey of chemicals used in the
textile  industry in 1977 estimates that 1
million kg of caustic was discharged from
cotton preparation processes  Much ad-
ditional caustic was used and recovered
by evaporation. The discharged caustic is
normally neutralized with acid  addition
and  discharged  to  a  municipal waste
treatment plant.
  The  objective  of  this  project was  to
demonstrate the use of hyperfiltration to
recover the caustic overflow from a scour
saturator.  The overflow  is too dirty for
reclamation by existing evaporators.
  The scope of this project included both
the operation  of an HF recovery system
coupled with  a full scale cotton scour
saturator and the determination of oper-
ating costs and technical feasibility of the
system as a means of reducing caustic
discharge from fabric preparation.

Project Results
  For 2 years HF membranes were oper-
ated with the overflow caustic (6 to 10
weight percent  NaOH) at  95°C from a
scour saturator in  a cotton preparation
range.  During  this  time,  the  caustic
discharge from this plant was reduced by
about 200,000 kg of NaOH.
  After initial operation of a pilot plant (10
m2 of membrane), a prototype unit (100
m2) was installed.  The prototype  unit
experienced corrosive problems in the
sintered  metal  membrane support.  A
properly prepared 316L grade stainless
steel module (7.2 m2) was installed and
operated successfully for over a year. The
entire 100 m2 prototype system was then
replaced with modules made of the new
material.
  The technical  feasibility of reuse of the
caustic was proven by the  production of
over 15 million m of approximately 1.5 m
wide fabric while recycling over 3 million
L of renovated  6 to  10 weight  percent
caustic (NaOH).
  Operating procedures were also devel-
oped. Daily washing was  established,
involving  a base-solvent  solution for
removing organics  and an acid  solution
for removing metallic oxides and hydrox-
ides.
  A  routine procedure for  completely
stripping and reforming membranes  in
place was also established. Details of the
membrane formation-in-place procedure
are proprietary.
  Operating costs, including labor and
chemicals for cleaning and a technology
support contract that provides  the time
and materials for membrane formation-
m-place, were established. The savings
of $379,900/yr yield a positive rate of
return  on the  $361,500 installed cost.
Annual operating costs are $37,900.
  These results led to an  expansion to
over 200 m2 of membrane area that  is
scheduled to begin operation in late 1985.
(Also, anHF unit of about 220m2 is being
installed to renovate mercerizer wash
water, 6 weight percent NaOH, for use as
dyehouse reagent.)
*1 Btu = 1 055 kj

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    C. A. Brandon is with CARRE, Inc., Seneca, SC 29679,
    John S. Ruppersberger is the EPA Project Officer fsee below}.
    The complete report,  entitled "Hyperfiltration for Textile Preparation Caustic
      Discharge Reduction," (Order No. PB 86-134 053/AS; Cost: $9.95, subject to
      change) will be available only from:
           National Technical Information Service
           5285 Port Royal Road
           Springfield, V'A 22161
           Telephone: 703-487-4650
    The EPA Project Officer can be contacted at:
           Air and Energy Engineering Research Laboratory
           U.S. Environmental Protection Agency
           Research Triangle Park. NC 27711
United States
Environmental Protection
Agency
                         Center for Environmental Research
                         Information
                         Cincinnati OH 45268
Official Business
Penalty for Private Use S300

EPA/600/S2-85/139
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