United States
                    Environmental Protection
                    Agency
Water Engineering
Research Laboratory
Cincinnati OH 45268
'/•'
 '/I
                    Research and Development
EPA/600/S2-85/140  Feb. 1986
&EPA          Project  Summary
                   Automation  of  Sludge
                   Processing:  Conditioning,
                   Dewatering,  and  Incineration

                   R. C. Polta, D. A. Stulc, and G. A. Mathes
                     This study developed and tested au-
                    tomated control strategies for munici-
                    pal wastewater sludge processing. The
                    strategies were applied to three unit
                    processes—chemical conditioning with
                    lime and ferric chloride, vacuum filtra-
                    tion, and incineration. The project was
                    conducted at the St. Paul, Minnesota,
                    Metropolitan Waste Control Commis-
                    sion (MWCC) Seneca facility, a 24-mgd
                    plant with parallel sludge processing
                    trains.
                     Several strategies were developed
                    for controlling lime and ferric chloride
                    addition and filter cake production rate.
                    Each strategy was evaluated during ap-
                    proximately 500 hr of operation.
                     Automated strategies were also de-
                    veloped for  controlling incinerator
                    hearth temperatures and air input. The
                    strategies were designed to maintain
                    the lowest possible furnace burning
                    zone and to minimize excess air. The
                    test data show a moderate cost reduc-
                    tion for automated control.
                     On-line sensors were used to collect
                    data and implement control strategies.
                    Performance data for these sensors are
                    summarized, and the digital data acqui-
                    sition and control system is described.

                     This Project Summary was devel-
                    oped by EPA's Water Engineering Re-
                    search Laboratory, Cincinnati, OH, to
                    announce key findings of the research
                    project that is fully described in a sepa-
                    rate report of the same title (see Project
                    Report ordering information at back).
                   Introduction
                     The costs for solids handling and dis-
                   posal at a conventional secondary treat-
ment facility are usually 30% to 50% of
the operating and maintenance (O & M)
budget. The solids handling processes
at a St. Paul,  Minnesota, Metropolitan
Waste Control Commission (MWCC)
treatment facility were studied to deter-
mine the impact of improved process
control on these costs. The primary goal
was to process the greatest volume of
sludge possible at the least cost. Proc-
ess control can be accomplished by
manual or automated means, but the
complexity and interaction of sludge
dewatering and incineration processes
limit manual control  to simplistic
schemes. In addition, the variable na-
ture of the raw sludge requires consid-
erable control flexibility. Thus auto-
matic digital control techniques were
used,

Study Objectives
  The overall study objective was to
model and eventually control the three
unit processes for  sludge treatment—
conditioning, dewatering, and incinera-
tion—to achieve near-optimum per-
formance for a particular operating
goal. This goal will change throughout
the year and may vary from maximizing
the volume of liquid sludge processed
to maintaining specified limits for par-
ticulates in the stack discharge. The
original reasoning was that if adequate
models could be generated, it would be
relatively easy to prepare an algorithm
to minimize the total cost for any given
operating scheme.  Though the overall
project objective was not met, the proj-
ect demonstrated that considerable cost
savings could be generated by using au-
tomated process control schemes even
when they are less than  optimum.

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Facility Operations
  All of the work described  was con-
ducted at the Seneca Wastewater Treat-
ment Plant on the Minnesota River in
Eagan, Minnesota. This facility has a de-
sign capacity of 90,840 m3/day (24
mgd).
  Approximately  10% of the influent
flow is  from industrial  sources. The
treatment  scheme consists of screen-
ing, grit removal, primary sedimenta-
tion, complete-mix activated sludge,
final sedimentation, and chlorination.
  The solids processing operations  in-
clude floatation thickening of waste-
activated sludge, vacuum filtration, and
incineration. Ferric chloride  and lime
are used to condition the sludge before
dewatering. All of the primary and
waste-activated sludges generated at
Seneca are processed along  with
sludges hauled from other MWCC facili-
ties. During 1980, the  plant processed
approximately 215,745  m3 (57  million
gallons) of liquid  sludge, of which ap-
proximately 93,490 m3 (24.7 million gal-
lons) were hauled to the plant.
  Because of the variable nature of the
raw sludge, the conditioning and filtra-
tion processes are extremely difficult to
operate at a steady output rate with a
cake of uniform burning characteristics.
The measured daily variation was 14%
to 25.5% for cake solids and 53% to 68%
for volatile solids. Filter yield varied by a
factor of three.
  Because  of the  lack of cake storage
capacity at Seneca, the incinerator must
burn the cake as produced, maintain
hearth  temperatures below 1100°C
(2000°F) to protect the furnace structure,
and meet air pollution standards. These
goals are difficult  to achieve  given the
variable nature of  the filter output.
  The total operating cost for sludge de-
watering and incineration at Seneca, in-
cluding  chemicals, energy, and labor,
was $166/metric ton ($151/ton) or ap-
proximately 47% of the total plant oper-
ating budget for 1981.

Chemical Conditioning Control
  To control chemical conditioning, it is
necessary to know the impact of chemi-
cal addition on the dewatering charac-
teristics of sludge. The two most com-
mon methods of estimating  sludge
dewaterability are  capillary suction time
(CST) and specific resistance  (SR).
  Ideally,  an  on-line  measurement
would  produce a  signal that could  be
used to vary the chemical dose and
maintain the desired dewatering char-
acteristics.  Unfortunately, neither CST
nor SR is directly measurable on-line.
However, a correlation was sought be-
tween CST or SR and other parameters
(Table 1) that could be measured on-
line.
  Rheological data were analyzed and
yielded a relationship between sludge
SR  (after conditioning with ferric chlo-
ride and lime) and several other sludge
parameters. This analysis  indicated the
feasibility of using on-line data to mea-
sure SR and CST.
  Because the conditioning process at
Seneca  uses  both  ferric  chloride and
lime, two control systems and  hence
two models were required. Since others
have demonstrated that SR adequately
describes sludge dewatering character-
istics for vacuum filtration, this parame-
ter  was selected for study.  Initial  at-
tempts  at determining the  SR  of
ferric-conditioned sludge yielded ex-
tremely  long filtration times, and in
most cases, no cake was formed. Since
the  laboratory  data demonstrated a
strong  relationship between the SR of
lime-conditioned sludge (SRL) and the
CST of lime-conditioned sludge (CSTL),
the CST of the ferric-conditioned  sludge
(CSTF) was used to characterize ferric
conditioning.
  The CST model was constructed with
a total of 124  data sets collected over a
7-month  period.  A  number of relation-
ships were developed to gauge the po-
tential for success and the need  for ad-
ditional data.  Multiple linear regression
analysis techniques were  used to ana-
lyze the data.
  The modeling  efforts resulted in the
following equations for predicting the
CST of  ferric-conditioned sludge
(R = 0.82).

  CST2 = 66-0.104(ORPD)         (1)

         - 1.8(PF) + 6.0(SSR)

         + 0.05 (ORPF) -  3.5 (PHD)

  The addition of the last  two variables
did little to improve the goodness of fit.
Thus for model CST2, 67% of the vari-
ability in the actual CST is explained by
the  independent variables. The unex-
plained variability may be related to the
measurement precision of the field
monitors or to one or more of the im-
portant (but unknown) parameters that
were not monitored.
  Three control schemes  were consid-
ered for  FeCI3 addition: pH (PHD) con-
trol, CST control, and sludge mass ratio
control. Tests demonstrated that both
the pH and the ORP sensors responded
to a change in FeCI3 dose, but that no
universal setpoint would maintain con-
slant  dewatering  characteristics. Thus
the feedback approach required addi-
tional parameters to make the strategy
responsive to sludge  conditioning
needs.
  Previous  experience  had demon-
strated that the FeCI3 dose required for
good vacuum filtration increased as the
raw sludge solids decreased. To reflect
this physical characteristic, the control
scheme was modified to calculate and
maintain PHD based on the raw sludge
solids concentration.

    PHD setpoint = K2 + 1C, (SSR)   (2)

and

 PHF setpoint = PHR - PHD setpoint (3)

  Test results demonstated that this
strategy could  control PHF. However,
the ability to maintain PHF at  the  set-
point did not insure  proper condition-
ing, as over- and under-dosing  resulted
when raw sludge characteristics other
than SSR changed. Proper conditioning
required manual entry of new values for
KT and K2. The control system was thus
reduced to  a semi-automated  scheme
requiring periodic judgments  by  the
operators.
  CST uses  a cascade control to adjust
the ferric pump. The inner loop  controls
the pH  of ferric-conditioned sludge by
adjusting pump speed. The pH setpoint
is generated by a CST controller.
  The model receives inputs from proc-
ess sensors  and predicts a CST value.  If
the prediction differs from the desired
value, a new pH setpoint value  is calcu-
lated. To avoid coupling problems, the
CST control model is recalculated infre-
quently, thereby appearing constant to
the pH controller.
  Evaluation of the on-line CST control
proved  a constant CST  setpoint to be
unworkable, as the FeCI3 pump ramped
to maximum or minimum speed if the
desired CST value was not attained.
Thus a variable CST setpoint  was ini-
tiated based on raw sludge solids.

    CST setpoint = K3 (SSR) - K4   (4)

  The variable CST setpoint provided  a
degree  of flexibility in the control strat-
egy,  but the constants  K3 and K4 re-
quired adjustment during control  runs
because of  changes  in sludge proper-
ties not totally reflected  in solids  con-

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 Table 1.    Sludge Modeling Parameters

 Symbol	
 Definition
 SSR         Suspended solids concentration in raw sludge, % solids
 PHR         pH of raw sludge
 PHF         pH of ferric-chloride-conditioned sludge
 PHL         pH of lime-conditioned sludge
 PHD         Differential pH
 ORP         Oxidation—reduction potential
 ORPR        ORP of raw sludge, mv
 ORPF        ORP of ferric-chloride-conditioned sludge, mv
 ORPL        ORP of lime-conditioned sludge, mv
 12          Shear stress of lime-conditioned sludge, 12 rpm, dyne/cm2.
 30          Shear stress of lime-conditioned sludge, 30 rpm, dyne/cm2.
 60          Shear stress of lime-conditioned sludge, 60 rpm, dyne/cm2.
 CST         Capillary suction time
 CSTR        CST of raw sludge, sec
 CSTF        CST of ferric-chloride-conditioned sludge, sec
 CSTL        CST of lime-conditioned sludge, sec
 SRL         Specific resistance of lime-conditioned sludge x  70~" m/kg
 SSL         Suspended solids concentration in lime-conditioned sludge, % solids
 TL          Temperature of lime-conditioned sludge, °C
 PF          Ferric chloride feed, % by weight of dry sludge solids
 PL          Lime feed, % by weight of dry sludge solids
 VAC         Vacuum in form zone, in. Hg
 VAT         Submergence of filter drum, in.
 DRUM       Rotational speed of filter drum, rph
 TPH         Wet cake production rate, ton/hr
 SSF         Total solids concentration in cake, % solids
 FLOW       Raw sludge flow, gpm
 CLOTH       Operating hours since media acid cleaned, hr
 SR3         Specific resistance of conditioned sludge calculated from the yield equation,
               m/kg	
 tent. Though the predicted CST closely
 followed the CST setpoint value, signifi-
 cant deviations between the setpoint pH
 and the measured pH remained.
  These problems were related  to the
 fouling of the  pH electrodes and
 changes in the sludge characteristics.
 Although short-term control was
 achieved  using the  model, a suitable
 setpoint for all sludges was not devel-
 oped.  Eventually, dose limits of 7% to
 13% FeCI3 were implemented to elimi-
 nate severe excursions.
  The  FeCI3 dose ratio control strategy
 is defined as follows:

  Ferric chloride mass flow =       (5)

  K5 (sludge mass flow) + K6 (SSR-4)

This control strategy uses a selected fer-
ric  chloride dose (K5) and reflects
changing sludge  characteristics
through K6. The advantages of the dose
ratio strategy  are that sensor mainte-
nance  is eliminated and a  given FeCI3
dose is maintained. Disadvantages are
that there  is no feedback adjustment,
that the accuracy of the sludge  solids
analyzer is critical, and that a steady-day
tank ferric chloride concentration is
required.
  A number of control schemes for lime
addition were  considered during the
course of the project, but the filter yield
dropped off dramatically when the pH
of the lime-conditioned sludge de-
creased much below 12.0. Thus the only
strategy used for the test runs was con-
trol of pH to 12.0 or  above.  Although
this strategy did not address the initial
intent of controlling the SR of the condi-
tioned sludge, it had two major advan-
tages:  It was simple and it worked.

Vacuum Filter Control

Control Strategies
  Initial filter control strategies were de-
signed to reduce the  variation in cake
yield and maximize the production rate
by stabilizing and controlling filter oper-
ating parameters.
  Analyses of vat level adjustments on
filter operation indicated that low vat
levels  and  higher drum speeds im-
proved cake quality  because of the
lower moisture content. However, to re-
duce the risk of vacuum loss and pro-
mote efficient cake release, most opera-
tors maintained the vat at high levels.
  Under  manual control, the vat level
varies in response to any change in the
filtration rate. For any  reasonable com-
 bination of parameters, the vat level
 reaches an equilibrium  value between
 the lower limit and the vat overflow.
 Any change in dewatering characteris-
 tics destroys this equilibrium, and the
 vat level changes to a new point.
   A cascade algorithm is used to control
 the vat level. The internal loop consists
 of a flow controller that adjusts the
 sludge pump motor speed. The external
 loop provides the flow setpoint.
   Only two variables that influence the
 cake production rate are adjustable: vat
 level and filter speed. Form zone vac-
 uum  is usually maintained  at the
 highest value possible.
   When automated control of the vat
 level and drum speed was initiated, the
 vat level setpoint was a function of the
 cake thickness.
                                           Vat level setpoint = K7 - K8

                                                x (thickness in inches/100)
                                   (6)
 Because attempts at thickness measure-
 ment  were not  successful, the cake
 thickness was calculated from the pro-
 duction rate, drum speed,  and cloth
 area.
   By judicious choice of the constants
 K7 and K8, reasonable setpoint values
 for a wide range of sludge characteris-
 tics can be established. The control ac-
 tion also reduces the chance of filter up-
 sets by increasing the level setpoint
 when lower cake production  rates (thin
 cakes)  occur because of  low sludge
 solids  or filter media blinding.
   Drum speed control used a cake pro-
 duction setpoint adjusted as a function
 of raw sludge solids concentration:

  Cake production setpoint = Kg    (7)

                     + K10 (SSR)

  A filter recovery mode was added,
 which  decreased the drum speed to a
 fixed value whenever cake production
 fell below a predetermined value, and
 an upper  limit was placed on the drum
 speed to prevent filter failure as a result
 of cake discharge problems. The upper
 limit also facilitated the use  of  a con-
 stant cake production setpoint without
 frequent upsets.

 Evaluation of Automated Vac-
 uum Filter Control
  Approximately  2800  hourly average
 data sets were generated for automated
 and manual filter control.  These data
 sets fell into three main categories: Data
3

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from filter No. 1 under computer con-
trol, data from filter No. 1 under manual
control, and data from filter No. 2 under
manual control.
  Performance data for the three modes
show that filter No.  1 under computer
control processed more  sludge with
lower chemical doses. If it is assumed
that the average raw sludge solids did
not vary for the three categories, then
the computer control mode also pro-
duced a drier cake.
  Although the wet cake yield was es-
sentially constant,  the variability of
chemical feed was considerably greater
in the manual  modes, especially for
lime.  These  data show that control of
the lime dose was the major advantage
of the computer control mode.
  In incineration operation, the ratio of
water to volatiles is important to fuel
consumption and steady hearth tem-
peratures. Although all attempts to esti-
mate  cake moisture  by direct and indi-
rect methods were  unsuccessful, this
ratio varied  more with  manual opera-
tions  and was  directly related to the
chemical  feed rates. Control of the
chemical feed systems would provide a
reasonably conditioned  sludge without
large  excursions in cake moisture and
volatile content. Table 2  summarizes
the average filter  performance by
mode.

Incinerator Control

Control Strategies
  Since the input to the incinerator can
vary,  even with automated control of
the dewatering  train, some control ac-
tion is necessary to maintain steady in-
cinerator operation. The primary objec-
tive for instituting new  incinerator
controls was to minimize the use of aux-
iliary  fuel  while burning all cake pro-
duced and  meeting stack discharge
standards.
  A series of tests was conducted to de-
termine whether the Seneca incinera-
tors could be operated  at rates near ca-
pacity and still meet the stack discharge
standard. The final control strategy was
based on these tests.
  This strategy used the calculated  in-
cinerator load as a feedforward signal.
This signal was delayed for each burn-
ing hearth to account for process dead-
time.  The temperatures on the con-
trolled hearths (Nos. 3, 5, and 6) were
used as feedback signals to tempera-
ture controllers. Fuel flow was in turn
regulated by the air flow rate. The tem-
perature controllers  received their set-
points from a temperature adjustment
supervisory program. The output from
the temperature controller was com-
bined with the delayed  loading signal at
adjustable ratios to throttle air valve po-
sitions. A burner sequence program
could start or stop the burners individu-
ally if necessary.  The temperature con-
trol program also prevented imbalances
between hearths.
  Furnace  pressure was controlled
using three signals—furnace load, fur-
nace draft, and atmospheric air damper
position—to calculate the position of
the induced-draft fan damper.
  The air for drying, burning, and cool-
ing was  provided through an  atmo-
spheric air damper on hearth No. 7 and
the return of the center shaft cooling air.
  The atmospheric air  damper was ad-
justed to maintain a fixed oxygen level
in the stack gas, and the incinerator load
was used as a feedforward trim. Hearth
temperatures are used  as a second trim
to detect conditions such as too much
cooling air entering the incinerator.
  In addition to the on-line sensors, vi-
sual observations are also required. For
example, dark smoke  indicates insuffi-
cient combustion air. Cake volatile
solids data are manually entered.
Table 2.   Average Filter Performance by Mode—Complete Sets
Parameter
Sludge feed. Us (gpm)
Cake yield, mt/hr (ton/hr)
Cake solids, %
Volatile solids, %
FeCly, % of sludge solids
CaO, % of sludge solids
pH of ferric cond. sludge
pH of lime cond. sludge
Ib H2O/lb volatile
Vat level, cm (in.)
Drum speed, rph
Filter No. 1
Computer
5.6 (89)
4.8 (5.3)
20.5
56
11.2
18.3
4.9
12.0
6.9
43 (17.1)
15.3

Manual
5.7 (90)
5.2 (5.7)
20.8
48
11.5
24.3
4.8
12.1
8.0
53 (21)
15.3
Filter No. 2
Manual
4.5 (71)
4.4 (4.8)
20.3
50
12.9
26.0
-
-
8.1
37 (14.8)
13.3
  Tests were conducted to characterize
the dynamic response of the process to
variations in temperature and gas flow.  A
The tests demonstrated that three dis-
tinct zones should  be maintained to
maximize fuel efficiency: cake drying on
hearth Nos. 1, 2, and 3, complete com-
bustion on hearth Nos. 4 and 5, and ash
cooling on hearth  Nos. 6 and 7. The
tests further determined that the above
zones could be maintained by operating
as follows:
  Furnace draft  	0.4 cm (0.15) H20
  Shaft cooling
    air 	  100% return to
                    hearth No. 7
  Ambient air	0-20% open as re-
                    quired
  Hearth 6 burner ..  Off
  Hearth 5 burner ..  100% capacity
  Hearth 3 burner ..  Control to 650°C
                    (1200°F)

  By eliminating burning on the upper
hearths, the thermal efficiency was in-
creased,  and  overall thermal  efficien-
cies of approximately 4420 kJ/kg (1900
BTU/lb) water evaporated could be ob-
tained. Typical values fell in the range of
4200 to 5800  kJ/kg  (1800 to 2500 BTU/
Ib).
  The  control strategy was organized
into two areas—temperature and gas
flow.  The recommended temperature
profile appears in Table 3. As previously
demonstrated,  these temperatures
could  be maintained without firing
hearth No. 6, only the burners on hearth
Nos. 3 and 5 were used regularly.
  Gas flow through the furnace was di-
vided into draft and oxygen control. The
draft  setpoint was manually entered,
and the controller adjusted the position
of the induced-draft fan damper.
  Gas flow through the  furnace was
controlled to  maintain a manually en-
tered value for flue gas oxygen concen-
tration. Tests indicated that all  shaft
cooling air should  be returned  to the
furnace  before opening the atmo-
spheric air  damper. This  goal was ac-
complished by using two independent
controllers. Subsequent tests demon-
strated that sufficient oxygen was usu-
ally obtained without opening the atmo-
spheric air damper.

Evaluation of Automated
Solids Processing
  Tests were conducted to  operate
process train No. 1 by computer and
process train No. 2 by hand. In one such
test, the initial setpoints for process
train No. 1 were as follows:

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                    Parameter
Wet cake yield 	
FeCI3 dose	
pH of lime-conditioned sludge
Incinerator draft	
Flue gas 02	
Hearth 2 temperature  	
Hearth 4 temperature  	
                     Setpoint

              5.4 mt/hr (6TPH)
              11% of dry sludge solids
              12.0
              5 mm (0.2  in.) H20
              7.4%
              565°C (1050T)
              980°C (1800°F)
  The performance data for the two de-
watering trains during the 11-hr test
No. 2 are summarized in Table 4. As in
other tests, the vacuum system limited
the performance of both trains. During
the ninth hour of the test, both filters
lost vacuum, were shut down, and were
restarted manually.
  Filter  No. 1 produced  a cake with a
higher volatile solids content, primarily
because of the reduced lime dose. The
FeCI3 dose in train No. 2 was lower than
normal because the actual discharge ca-
pacity of the chemical feed pump was
only 45% of its nominal capacity.
  The fuel efficiencies of the two proc-
ess trains are summarized in Table 5.
The total energy used per mass of water
fed was significantly lower than normal
for both trains, but because of the
higher volatile content, furnace No. 1
was  more efficient.
  The improvement in the efficiency of
furnace No. 1 can be attributed to set-
ting  an upper temperature limit for
hearth No. 4. Initially  this limit was
980°C (1800°F), and  it was changed to
950°C (1750°F) at 1610 hr.
  The results show that automated con-
trol of solids processing can yield eco-
nomic savings. For Seneca, the annual
savings are estimated to be $50,000 for
chemicals and $48,000 to $127,000 for
energy, depending on whether natural
gas or oil is used.

Recommendations

Control Strategy for Sludge
Conditioning
  Changes in the raw sludge character-
istics have a dramatic impact on the per-
formance of a vacuum filter and, subse-
quently, the incinerator. Thus operators
tend to include a significant factor of
safety when selecting dose rates for
chemical  conditioning. This project
demonstrated the need for an on-line
method of identifying the dewatering
characteristics of chemically condi-
tioned  sludge. However, since such a
method is not presently available, the
recommended control strategy is out-
lined as follows:
  1.  FeCI3—Maintain a constant dose
     of 6% to 12% of dry solids. The
     specific dose is a function  of the
     raw sludge variability and the op-
     erator time available to monitor fil-
     ter operation.
  2.  Lime—Maintain a constant pH of
     12 for Seneca after lime addition.
     The above strategies require only
     three field sensors—raw sludge
     flow,  raw sludge solids, and lime-
     conditioned sludge pH.

Control Strategy for Sludge
Dewatering
  The operating  strategy is based on
the assumption that the dry yield of
sludge processing must be maximized.
Because an on-line cake moisture ana-
lyzer was not found, the recommended
strategy is based on maximizing the wet
cake yield  without exceeding the incin-
erator capacity. After selecting the wet
cake yield setpoint the recommended
strategy is as follows:
  1.  Yield—Adjust the drum speed to
     obtain the yield; however, to main-
     tain a reasonable cake thickness,
     apply an upper limit of 18 rph.
     When the yield is below  setpoint,
     the drum speed will increase to in-
     crease yield. As the drum speed in-
     creases, the cake thickness will de-
     crease.  To  eliminate problems
     with  a thin cake, the following
     equation is used to calculate a new
     vat level setpoint:

    Vat level  setpoint = K7 - K8

                      x (thickness)

     Increased vat level will  increase
     cake thickness.
  2.  Vat Level—The vat level  is main-
     tained by varying the raw sludge
     flow rate, which in turn causes the
     feed rate of FeCI3 to vary.
To implement this strategy, the opera-
tor must enter the setpoint value for
yield along with the constants K9 and
KIQ.
  Once  the conditioning  strategy is
adopted, the  dewatering strategy re-
quires only three additional sensors—a
belt  scale to determine cake yield, a
level detector to measure vat level, and
a tachometer to determine drum speed.

Incinerator Control Strategy
  The recommended incinerator con-
trol strategy is divided into the follow-
ing two areas:
  1.  Temperature—Only the burners
     on hearth Nos. 3 and 5 are used in
     this strategy. Hearth No. 3 burners
     are operated to maintain a temper-
     ature of approximately 540°C
     (1000°F) on  hearth No. 2, and the
     burners on  hearth No. 5 are con-
     trolled to maintain a temperature
     of approximately 950°C (1750°F) on
     hearth No. 4. For the typical load-
     ing rates observed  at  Seneca,
     these setpoints make hearth No. 4
     the main burning hearth.
  2.  Air Flow—The air flow strategy
     consists of  maintaining the  fur-
     nace pressure in the  range of
     -0.38 to -0.51 cm (-0.15 to -.20
     in.) H2O. For cake loadings below
     approximately 4.1  wet mt/hr  (4.5
     wet ton/hr), the lower  (absolute
     value)  setpoint is sufficient.  A
     lower limit of approximately 20%
     open should be established for the
     induced-draft damper. This  limit
     will prevent problems associated
     with  low draft values. The atmos-
     pheric  air damper should remain
     closed, and all air not entering at the
     burners or through uncontrollable
     leaks should be provided as recycled
     shaft cooling air. The flow of re-
     cycled cooling air should be con-
     trolled to maintain the desired O2
     concentration on hearth No. 1. The
     Oz setpoint  should be determined
     from visual  observation on hearth
     Nos.  1 through 4. Sufficient  O2
     should be  provided to  minimize
     smoke generation.
  During the test, it appeared that air
may have entered through the sludge
feed drop gate at  the top of the incinera-
tor. For this reason, the O2 concentra-
tion  should be determined on hearth
No.  1 as opposed to the downstream
location used during the tests. Also, a
continuous measurement of opacity
should be used to provide feedback for
adjusting the oxygen setpoint or the fil-
ter yield or both.
  The incinerator control strategy uses
the standard temperature and pressure
sensors found on most furnaces. In ad-
dition to these instruments, an oxygen
analyzer is required on hearth No. 1.
5

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Summary and Conclusions
  The study demonstrated that automa-
tion of the sludge treatment facilities at
the Seneca plant would yield annual
savings on the order of $100,000 based
on 1981 costs for conditioning chemi-
cals and fuel. This estimate is based on
implementation of the following control
strategies:
  1.  Control of the chemical condition-
     ing process consists of maintain-
     ing an FeCI3 dose in the range of
     6% to 12% (based  on  dry sludge
     solids) and adding  sufficient lime
     to maintain a pH of 12.0.
  2.  The  vacuum  filter yield (wet
     weight/time) is controlled by ad-
     justing the drum speed. Vat level is
     adjusted to maintain a cake thick
     enough to discharge properly.
     Level is maintained  by varying raw
     sludge flow rate,  which in turn
     varies the chemical feed rates.
  3.  The hearth temperatures are ap-
     proximately 540°C (1000°F) on
     No. 2 and 950°C (1750°F) on No. 4.
     Temperature is controlled by ma-
     nipulating the  burners on  hearth
     Nos. 3 and 5, respectively. Furnace
     pressure is maintained at -0.38 to
     -0.51 cm  (-0.15 to -0.20 in.) by
     manipulating the induced-draft fan
     damper. The flow of recycled cool-
     ing air is controlled to maintain a
     setpoint oxygen concentration in
     hearth No. 1. Additional air is gen-
     erally not required.

  The following is a summary of the
performance of the sensors used during
this study:
Table 3.    Recommended Temperature Profile for Controlled Incineration

                                        Temperature, °C (°F)
Hearth No.
1
2
3
4
5
6
7
Minimum
400 (750)
450 (850)
650 (1200)
760 (1400)
590(1100)
200 (400)
80 (180)
Average
430 (800)
480 (900)
700 (1300)
870 (1600)
650 (1200)
260 (500)
90 (200)
Maximum
450 (850)
540 (1000)
760 (1400)
980 (1800)
700 (1300)
310 (600)
90 (200)
Table 4.    Dewatering Performance During Test No. 2
Parameter
Hours
Sludge flow, Us (gpm)
Raw sludge solids, %
FeC/a, %
CaO, %
Yield, wet mt/hr (TPH)
Cake solids, %
Cake volatile solids, %
Process Train
No. 1 (Computer)
11
4.4 (70)
4.1
11
18
4.7
20.5
53.8
Process Train
No. 2 (Manual)
11
4.2 (66)
4.1
8.5
25
4.4 (4.9)
21.2
44.1
Parameter
Hours
Gas use, sm3/hr (SCFH)
Gas use, sm3/wet mt (SCF/wet ton)
Gas use, sm3/dry mt (SCF/dry ton)
Total energy, kJ/kg H^ (BTU/lb H2O)
Gas, kJ/kg H2O (BTU/lb H£»
Process Train
No. 1 (Computer)
11
184 (6,500)
39 (1,250)
184 (5,900)
4,885(2,100)
1,860 (800)
Process Train
No. 2 (Manual)
11
218 (7,700)
50 (1,600)
240 (7,700)
4,885(2,100)
2,325 (1,000)
Acceptable
Vat level
Temperature
Rotational speed
Rotational position
Sludge flow

pH
Solids
Vacuum
Cake weight
Questionable
ORP
Oxygen
Turbidity
Unacceptable
Viscosity
Cake thickness
Cake moisture
Tank level
                                                                              sorship of the U.S. Environmental Pro-
                                                                              tection Agency.
  Several studies  were conducted at
Seneca to determine whether commer-
cially available sensors could provide a
continuous measure of cake moisture.
All those tested were  unacceptable, as
they failed to provide reliable estimates
of cake moisture.
  Even acceptable  sensors require sig-
nificant maintenance. The extreme is
the conditioned  sludge pH sensor,
which  required cleaning at least once
per shift. Although  the maintenance re-
quired for the other sensors was lower.
both the raw sludge solids sensor and
the belt scale require frequent calibra-
tion to  assure success of the control
system.
  Control of sludge-handling processes
should be designed to allow operator-
entered setpoints to maintain operation
without going to complete manual
operation.
  The full report was submitted in fulfill-
ment of Grant  No. S803602 by the
Metropolitan Waste Control Commis-
sion of St. Paul, Minnesota, under spon-
                                                                       •&U. S. GOVERNMENT PRINTING OFFICE:!986/646-116/20775

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    R, C. Polta and D. A. Stulc are with the Metropolitan Waste Control Commission,
      St. Paul. MN 55101; and G. A. Mathes is with EMA, Inc., St. Paul. MM 55101.
    Waiter W. Schuk is the EPA Project Officer (see below).
    The complete report, entitled "Automation of Sludge Processing: Conditioning,
      Dewatering, and Incineration," (Order No. PB 86-138 963/AS; Cost: $22.95.
      subject to change) will be available only from:
            National Technical Information Service
            5285 Port Royal Road
            Springfield, VA2216J
            Telephone: 703-487-4650
    The EPA Project Officer can be contacted at:
            Water Engineering Research Laboratory
            U.S. Environmental Protection Agency
            Cincinnati. OH 45268
United States
Environmental Protection
Agency
Center for Environmental Research
Information
Cincinnati OH 45268
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