United States Environmental Protection Agency Water Engineering Research Laboratory Cincinnati OH 45268 '/•' '/I Research and Development EPA/600/S2-85/140 Feb. 1986 &EPA Project Summary Automation of Sludge Processing: Conditioning, Dewatering, and Incineration R. C. Polta, D. A. Stulc, and G. A. Mathes This study developed and tested au- tomated control strategies for munici- pal wastewater sludge processing. The strategies were applied to three unit processes—chemical conditioning with lime and ferric chloride, vacuum filtra- tion, and incineration. The project was conducted at the St. Paul, Minnesota, Metropolitan Waste Control Commis- sion (MWCC) Seneca facility, a 24-mgd plant with parallel sludge processing trains. Several strategies were developed for controlling lime and ferric chloride addition and filter cake production rate. Each strategy was evaluated during ap- proximately 500 hr of operation. Automated strategies were also de- veloped for controlling incinerator hearth temperatures and air input. The strategies were designed to maintain the lowest possible furnace burning zone and to minimize excess air. The test data show a moderate cost reduc- tion for automated control. On-line sensors were used to collect data and implement control strategies. Performance data for these sensors are summarized, and the digital data acqui- sition and control system is described. This Project Summary was devel- oped by EPA's Water Engineering Re- search Laboratory, Cincinnati, OH, to announce key findings of the research project that is fully described in a sepa- rate report of the same title (see Project Report ordering information at back). Introduction The costs for solids handling and dis- posal at a conventional secondary treat- ment facility are usually 30% to 50% of the operating and maintenance (O & M) budget. The solids handling processes at a St. Paul, Minnesota, Metropolitan Waste Control Commission (MWCC) treatment facility were studied to deter- mine the impact of improved process control on these costs. The primary goal was to process the greatest volume of sludge possible at the least cost. Proc- ess control can be accomplished by manual or automated means, but the complexity and interaction of sludge dewatering and incineration processes limit manual control to simplistic schemes. In addition, the variable na- ture of the raw sludge requires consid- erable control flexibility. Thus auto- matic digital control techniques were used, Study Objectives The overall study objective was to model and eventually control the three unit processes for sludge treatment— conditioning, dewatering, and incinera- tion—to achieve near-optimum per- formance for a particular operating goal. This goal will change throughout the year and may vary from maximizing the volume of liquid sludge processed to maintaining specified limits for par- ticulates in the stack discharge. The original reasoning was that if adequate models could be generated, it would be relatively easy to prepare an algorithm to minimize the total cost for any given operating scheme. Though the overall project objective was not met, the proj- ect demonstrated that considerable cost savings could be generated by using au- tomated process control schemes even when they are less than optimum. ------- Facility Operations All of the work described was con- ducted at the Seneca Wastewater Treat- ment Plant on the Minnesota River in Eagan, Minnesota. This facility has a de- sign capacity of 90,840 m3/day (24 mgd). Approximately 10% of the influent flow is from industrial sources. The treatment scheme consists of screen- ing, grit removal, primary sedimenta- tion, complete-mix activated sludge, final sedimentation, and chlorination. The solids processing operations in- clude floatation thickening of waste- activated sludge, vacuum filtration, and incineration. Ferric chloride and lime are used to condition the sludge before dewatering. All of the primary and waste-activated sludges generated at Seneca are processed along with sludges hauled from other MWCC facili- ties. During 1980, the plant processed approximately 215,745 m3 (57 million gallons) of liquid sludge, of which ap- proximately 93,490 m3 (24.7 million gal- lons) were hauled to the plant. Because of the variable nature of the raw sludge, the conditioning and filtra- tion processes are extremely difficult to operate at a steady output rate with a cake of uniform burning characteristics. The measured daily variation was 14% to 25.5% for cake solids and 53% to 68% for volatile solids. Filter yield varied by a factor of three. Because of the lack of cake storage capacity at Seneca, the incinerator must burn the cake as produced, maintain hearth temperatures below 1100°C (2000°F) to protect the furnace structure, and meet air pollution standards. These goals are difficult to achieve given the variable nature of the filter output. The total operating cost for sludge de- watering and incineration at Seneca, in- cluding chemicals, energy, and labor, was $166/metric ton ($151/ton) or ap- proximately 47% of the total plant oper- ating budget for 1981. Chemical Conditioning Control To control chemical conditioning, it is necessary to know the impact of chemi- cal addition on the dewatering charac- teristics of sludge. The two most com- mon methods of estimating sludge dewaterability are capillary suction time (CST) and specific resistance (SR). Ideally, an on-line measurement would produce a signal that could be used to vary the chemical dose and maintain the desired dewatering char- acteristics. Unfortunately, neither CST nor SR is directly measurable on-line. However, a correlation was sought be- tween CST or SR and other parameters (Table 1) that could be measured on- line. Rheological data were analyzed and yielded a relationship between sludge SR (after conditioning with ferric chlo- ride and lime) and several other sludge parameters. This analysis indicated the feasibility of using on-line data to mea- sure SR and CST. Because the conditioning process at Seneca uses both ferric chloride and lime, two control systems and hence two models were required. Since others have demonstrated that SR adequately describes sludge dewatering character- istics for vacuum filtration, this parame- ter was selected for study. Initial at- tempts at determining the SR of ferric-conditioned sludge yielded ex- tremely long filtration times, and in most cases, no cake was formed. Since the laboratory data demonstrated a strong relationship between the SR of lime-conditioned sludge (SRL) and the CST of lime-conditioned sludge (CSTL), the CST of the ferric-conditioned sludge (CSTF) was used to characterize ferric conditioning. The CST model was constructed with a total of 124 data sets collected over a 7-month period. A number of relation- ships were developed to gauge the po- tential for success and the need for ad- ditional data. Multiple linear regression analysis techniques were used to ana- lyze the data. The modeling efforts resulted in the following equations for predicting the CST of ferric-conditioned sludge (R = 0.82). CST2 = 66-0.104(ORPD) (1) - 1.8(PF) + 6.0(SSR) + 0.05 (ORPF) - 3.5 (PHD) The addition of the last two variables did little to improve the goodness of fit. Thus for model CST2, 67% of the vari- ability in the actual CST is explained by the independent variables. The unex- plained variability may be related to the measurement precision of the field monitors or to one or more of the im- portant (but unknown) parameters that were not monitored. Three control schemes were consid- ered for FeCI3 addition: pH (PHD) con- trol, CST control, and sludge mass ratio control. Tests demonstrated that both the pH and the ORP sensors responded to a change in FeCI3 dose, but that no universal setpoint would maintain con- slant dewatering characteristics. Thus the feedback approach required addi- tional parameters to make the strategy responsive to sludge conditioning needs. Previous experience had demon- strated that the FeCI3 dose required for good vacuum filtration increased as the raw sludge solids decreased. To reflect this physical characteristic, the control scheme was modified to calculate and maintain PHD based on the raw sludge solids concentration. PHD setpoint = K2 + 1C, (SSR) (2) and PHF setpoint = PHR - PHD setpoint (3) Test results demonstated that this strategy could control PHF. However, the ability to maintain PHF at the set- point did not insure proper condition- ing, as over- and under-dosing resulted when raw sludge characteristics other than SSR changed. Proper conditioning required manual entry of new values for KT and K2. The control system was thus reduced to a semi-automated scheme requiring periodic judgments by the operators. CST uses a cascade control to adjust the ferric pump. The inner loop controls the pH of ferric-conditioned sludge by adjusting pump speed. The pH setpoint is generated by a CST controller. The model receives inputs from proc- ess sensors and predicts a CST value. If the prediction differs from the desired value, a new pH setpoint value is calcu- lated. To avoid coupling problems, the CST control model is recalculated infre- quently, thereby appearing constant to the pH controller. Evaluation of the on-line CST control proved a constant CST setpoint to be unworkable, as the FeCI3 pump ramped to maximum or minimum speed if the desired CST value was not attained. Thus a variable CST setpoint was ini- tiated based on raw sludge solids. CST setpoint = K3 (SSR) - K4 (4) The variable CST setpoint provided a degree of flexibility in the control strat- egy, but the constants K3 and K4 re- quired adjustment during control runs because of changes in sludge proper- ties not totally reflected in solids con- ------- Table 1. Sludge Modeling Parameters Symbol Definition SSR Suspended solids concentration in raw sludge, % solids PHR pH of raw sludge PHF pH of ferric-chloride-conditioned sludge PHL pH of lime-conditioned sludge PHD Differential pH ORP Oxidation—reduction potential ORPR ORP of raw sludge, mv ORPF ORP of ferric-chloride-conditioned sludge, mv ORPL ORP of lime-conditioned sludge, mv 12 Shear stress of lime-conditioned sludge, 12 rpm, dyne/cm2. 30 Shear stress of lime-conditioned sludge, 30 rpm, dyne/cm2. 60 Shear stress of lime-conditioned sludge, 60 rpm, dyne/cm2. CST Capillary suction time CSTR CST of raw sludge, sec CSTF CST of ferric-chloride-conditioned sludge, sec CSTL CST of lime-conditioned sludge, sec SRL Specific resistance of lime-conditioned sludge x 70~" m/kg SSL Suspended solids concentration in lime-conditioned sludge, % solids TL Temperature of lime-conditioned sludge, °C PF Ferric chloride feed, % by weight of dry sludge solids PL Lime feed, % by weight of dry sludge solids VAC Vacuum in form zone, in. Hg VAT Submergence of filter drum, in. DRUM Rotational speed of filter drum, rph TPH Wet cake production rate, ton/hr SSF Total solids concentration in cake, % solids FLOW Raw sludge flow, gpm CLOTH Operating hours since media acid cleaned, hr SR3 Specific resistance of conditioned sludge calculated from the yield equation, m/kg tent. Though the predicted CST closely followed the CST setpoint value, signifi- cant deviations between the setpoint pH and the measured pH remained. These problems were related to the fouling of the pH electrodes and changes in the sludge characteristics. Although short-term control was achieved using the model, a suitable setpoint for all sludges was not devel- oped. Eventually, dose limits of 7% to 13% FeCI3 were implemented to elimi- nate severe excursions. The FeCI3 dose ratio control strategy is defined as follows: Ferric chloride mass flow = (5) K5 (sludge mass flow) + K6 (SSR-4) This control strategy uses a selected fer- ric chloride dose (K5) and reflects changing sludge characteristics through K6. The advantages of the dose ratio strategy are that sensor mainte- nance is eliminated and a given FeCI3 dose is maintained. Disadvantages are that there is no feedback adjustment, that the accuracy of the sludge solids analyzer is critical, and that a steady-day tank ferric chloride concentration is required. A number of control schemes for lime addition were considered during the course of the project, but the filter yield dropped off dramatically when the pH of the lime-conditioned sludge de- creased much below 12.0. Thus the only strategy used for the test runs was con- trol of pH to 12.0 or above. Although this strategy did not address the initial intent of controlling the SR of the condi- tioned sludge, it had two major advan- tages: It was simple and it worked. Vacuum Filter Control Control Strategies Initial filter control strategies were de- signed to reduce the variation in cake yield and maximize the production rate by stabilizing and controlling filter oper- ating parameters. Analyses of vat level adjustments on filter operation indicated that low vat levels and higher drum speeds im- proved cake quality because of the lower moisture content. However, to re- duce the risk of vacuum loss and pro- mote efficient cake release, most opera- tors maintained the vat at high levels. Under manual control, the vat level varies in response to any change in the filtration rate. For any reasonable com- bination of parameters, the vat level reaches an equilibrium value between the lower limit and the vat overflow. Any change in dewatering characteris- tics destroys this equilibrium, and the vat level changes to a new point. A cascade algorithm is used to control the vat level. The internal loop consists of a flow controller that adjusts the sludge pump motor speed. The external loop provides the flow setpoint. Only two variables that influence the cake production rate are adjustable: vat level and filter speed. Form zone vac- uum is usually maintained at the highest value possible. When automated control of the vat level and drum speed was initiated, the vat level setpoint was a function of the cake thickness. Vat level setpoint = K7 - K8 x (thickness in inches/100) (6) Because attempts at thickness measure- ment were not successful, the cake thickness was calculated from the pro- duction rate, drum speed, and cloth area. By judicious choice of the constants K7 and K8, reasonable setpoint values for a wide range of sludge characteris- tics can be established. The control ac- tion also reduces the chance of filter up- sets by increasing the level setpoint when lower cake production rates (thin cakes) occur because of low sludge solids or filter media blinding. Drum speed control used a cake pro- duction setpoint adjusted as a function of raw sludge solids concentration: Cake production setpoint = Kg (7) + K10 (SSR) A filter recovery mode was added, which decreased the drum speed to a fixed value whenever cake production fell below a predetermined value, and an upper limit was placed on the drum speed to prevent filter failure as a result of cake discharge problems. The upper limit also facilitated the use of a con- stant cake production setpoint without frequent upsets. Evaluation of Automated Vac- uum Filter Control Approximately 2800 hourly average data sets were generated for automated and manual filter control. These data sets fell into three main categories: Data 3 ------- from filter No. 1 under computer con- trol, data from filter No. 1 under manual control, and data from filter No. 2 under manual control. Performance data for the three modes show that filter No. 1 under computer control processed more sludge with lower chemical doses. If it is assumed that the average raw sludge solids did not vary for the three categories, then the computer control mode also pro- duced a drier cake. Although the wet cake yield was es- sentially constant, the variability of chemical feed was considerably greater in the manual modes, especially for lime. These data show that control of the lime dose was the major advantage of the computer control mode. In incineration operation, the ratio of water to volatiles is important to fuel consumption and steady hearth tem- peratures. Although all attempts to esti- mate cake moisture by direct and indi- rect methods were unsuccessful, this ratio varied more with manual opera- tions and was directly related to the chemical feed rates. Control of the chemical feed systems would provide a reasonably conditioned sludge without large excursions in cake moisture and volatile content. Table 2 summarizes the average filter performance by mode. Incinerator Control Control Strategies Since the input to the incinerator can vary, even with automated control of the dewatering train, some control ac- tion is necessary to maintain steady in- cinerator operation. The primary objec- tive for instituting new incinerator controls was to minimize the use of aux- iliary fuel while burning all cake pro- duced and meeting stack discharge standards. A series of tests was conducted to de- termine whether the Seneca incinera- tors could be operated at rates near ca- pacity and still meet the stack discharge standard. The final control strategy was based on these tests. This strategy used the calculated in- cinerator load as a feedforward signal. This signal was delayed for each burn- ing hearth to account for process dead- time. The temperatures on the con- trolled hearths (Nos. 3, 5, and 6) were used as feedback signals to tempera- ture controllers. Fuel flow was in turn regulated by the air flow rate. The tem- perature controllers received their set- points from a temperature adjustment supervisory program. The output from the temperature controller was com- bined with the delayed loading signal at adjustable ratios to throttle air valve po- sitions. A burner sequence program could start or stop the burners individu- ally if necessary. The temperature con- trol program also prevented imbalances between hearths. Furnace pressure was controlled using three signals—furnace load, fur- nace draft, and atmospheric air damper position—to calculate the position of the induced-draft fan damper. The air for drying, burning, and cool- ing was provided through an atmo- spheric air damper on hearth No. 7 and the return of the center shaft cooling air. The atmospheric air damper was ad- justed to maintain a fixed oxygen level in the stack gas, and the incinerator load was used as a feedforward trim. Hearth temperatures are used as a second trim to detect conditions such as too much cooling air entering the incinerator. In addition to the on-line sensors, vi- sual observations are also required. For example, dark smoke indicates insuffi- cient combustion air. Cake volatile solids data are manually entered. Table 2. Average Filter Performance by Mode—Complete Sets Parameter Sludge feed. Us (gpm) Cake yield, mt/hr (ton/hr) Cake solids, % Volatile solids, % FeCly, % of sludge solids CaO, % of sludge solids pH of ferric cond. sludge pH of lime cond. sludge Ib H2O/lb volatile Vat level, cm (in.) Drum speed, rph Filter No. 1 Computer 5.6 (89) 4.8 (5.3) 20.5 56 11.2 18.3 4.9 12.0 6.9 43 (17.1) 15.3 Manual 5.7 (90) 5.2 (5.7) 20.8 48 11.5 24.3 4.8 12.1 8.0 53 (21) 15.3 Filter No. 2 Manual 4.5 (71) 4.4 (4.8) 20.3 50 12.9 26.0 - - 8.1 37 (14.8) 13.3 Tests were conducted to characterize the dynamic response of the process to variations in temperature and gas flow. A The tests demonstrated that three dis- tinct zones should be maintained to maximize fuel efficiency: cake drying on hearth Nos. 1, 2, and 3, complete com- bustion on hearth Nos. 4 and 5, and ash cooling on hearth Nos. 6 and 7. The tests further determined that the above zones could be maintained by operating as follows: Furnace draft 0.4 cm (0.15) H20 Shaft cooling air 100% return to hearth No. 7 Ambient air 0-20% open as re- quired Hearth 6 burner .. Off Hearth 5 burner .. 100% capacity Hearth 3 burner .. Control to 650°C (1200°F) By eliminating burning on the upper hearths, the thermal efficiency was in- creased, and overall thermal efficien- cies of approximately 4420 kJ/kg (1900 BTU/lb) water evaporated could be ob- tained. Typical values fell in the range of 4200 to 5800 kJ/kg (1800 to 2500 BTU/ Ib). The control strategy was organized into two areas—temperature and gas flow. The recommended temperature profile appears in Table 3. As previously demonstrated, these temperatures could be maintained without firing hearth No. 6, only the burners on hearth Nos. 3 and 5 were used regularly. Gas flow through the furnace was di- vided into draft and oxygen control. The draft setpoint was manually entered, and the controller adjusted the position of the induced-draft fan damper. Gas flow through the furnace was controlled to maintain a manually en- tered value for flue gas oxygen concen- tration. Tests indicated that all shaft cooling air should be returned to the furnace before opening the atmo- spheric air damper. This goal was ac- complished by using two independent controllers. Subsequent tests demon- strated that sufficient oxygen was usu- ally obtained without opening the atmo- spheric air damper. Evaluation of Automated Solids Processing Tests were conducted to operate process train No. 1 by computer and process train No. 2 by hand. In one such test, the initial setpoints for process train No. 1 were as follows: ------- Parameter Wet cake yield FeCI3 dose pH of lime-conditioned sludge Incinerator draft Flue gas 02 Hearth 2 temperature Hearth 4 temperature Setpoint 5.4 mt/hr (6TPH) 11% of dry sludge solids 12.0 5 mm (0.2 in.) H20 7.4% 565°C (1050T) 980°C (1800°F) The performance data for the two de- watering trains during the 11-hr test No. 2 are summarized in Table 4. As in other tests, the vacuum system limited the performance of both trains. During the ninth hour of the test, both filters lost vacuum, were shut down, and were restarted manually. Filter No. 1 produced a cake with a higher volatile solids content, primarily because of the reduced lime dose. The FeCI3 dose in train No. 2 was lower than normal because the actual discharge ca- pacity of the chemical feed pump was only 45% of its nominal capacity. The fuel efficiencies of the two proc- ess trains are summarized in Table 5. The total energy used per mass of water fed was significantly lower than normal for both trains, but because of the higher volatile content, furnace No. 1 was more efficient. The improvement in the efficiency of furnace No. 1 can be attributed to set- ting an upper temperature limit for hearth No. 4. Initially this limit was 980°C (1800°F), and it was changed to 950°C (1750°F) at 1610 hr. The results show that automated con- trol of solids processing can yield eco- nomic savings. For Seneca, the annual savings are estimated to be $50,000 for chemicals and $48,000 to $127,000 for energy, depending on whether natural gas or oil is used. Recommendations Control Strategy for Sludge Conditioning Changes in the raw sludge character- istics have a dramatic impact on the per- formance of a vacuum filter and, subse- quently, the incinerator. Thus operators tend to include a significant factor of safety when selecting dose rates for chemical conditioning. This project demonstrated the need for an on-line method of identifying the dewatering characteristics of chemically condi- tioned sludge. However, since such a method is not presently available, the recommended control strategy is out- lined as follows: 1. FeCI3—Maintain a constant dose of 6% to 12% of dry solids. The specific dose is a function of the raw sludge variability and the op- erator time available to monitor fil- ter operation. 2. Lime—Maintain a constant pH of 12 for Seneca after lime addition. The above strategies require only three field sensors—raw sludge flow, raw sludge solids, and lime- conditioned sludge pH. Control Strategy for Sludge Dewatering The operating strategy is based on the assumption that the dry yield of sludge processing must be maximized. Because an on-line cake moisture ana- lyzer was not found, the recommended strategy is based on maximizing the wet cake yield without exceeding the incin- erator capacity. After selecting the wet cake yield setpoint the recommended strategy is as follows: 1. Yield—Adjust the drum speed to obtain the yield; however, to main- tain a reasonable cake thickness, apply an upper limit of 18 rph. When the yield is below setpoint, the drum speed will increase to in- crease yield. As the drum speed in- creases, the cake thickness will de- crease. To eliminate problems with a thin cake, the following equation is used to calculate a new vat level setpoint: Vat level setpoint = K7 - K8 x (thickness) Increased vat level will increase cake thickness. 2. Vat Level—The vat level is main- tained by varying the raw sludge flow rate, which in turn causes the feed rate of FeCI3 to vary. To implement this strategy, the opera- tor must enter the setpoint value for yield along with the constants K9 and KIQ. Once the conditioning strategy is adopted, the dewatering strategy re- quires only three additional sensors—a belt scale to determine cake yield, a level detector to measure vat level, and a tachometer to determine drum speed. Incinerator Control Strategy The recommended incinerator con- trol strategy is divided into the follow- ing two areas: 1. Temperature—Only the burners on hearth Nos. 3 and 5 are used in this strategy. Hearth No. 3 burners are operated to maintain a temper- ature of approximately 540°C (1000°F) on hearth No. 2, and the burners on hearth No. 5 are con- trolled to maintain a temperature of approximately 950°C (1750°F) on hearth No. 4. For the typical load- ing rates observed at Seneca, these setpoints make hearth No. 4 the main burning hearth. 2. Air Flow—The air flow strategy consists of maintaining the fur- nace pressure in the range of -0.38 to -0.51 cm (-0.15 to -.20 in.) H2O. For cake loadings below approximately 4.1 wet mt/hr (4.5 wet ton/hr), the lower (absolute value) setpoint is sufficient. A lower limit of approximately 20% open should be established for the induced-draft damper. This limit will prevent problems associated with low draft values. The atmos- pheric air damper should remain closed, and all air not entering at the burners or through uncontrollable leaks should be provided as recycled shaft cooling air. The flow of re- cycled cooling air should be con- trolled to maintain the desired O2 concentration on hearth No. 1. The Oz setpoint should be determined from visual observation on hearth Nos. 1 through 4. Sufficient O2 should be provided to minimize smoke generation. During the test, it appeared that air may have entered through the sludge feed drop gate at the top of the incinera- tor. For this reason, the O2 concentra- tion should be determined on hearth No. 1 as opposed to the downstream location used during the tests. Also, a continuous measurement of opacity should be used to provide feedback for adjusting the oxygen setpoint or the fil- ter yield or both. The incinerator control strategy uses the standard temperature and pressure sensors found on most furnaces. In ad- dition to these instruments, an oxygen analyzer is required on hearth No. 1. 5 ------- Summary and Conclusions The study demonstrated that automa- tion of the sludge treatment facilities at the Seneca plant would yield annual savings on the order of $100,000 based on 1981 costs for conditioning chemi- cals and fuel. This estimate is based on implementation of the following control strategies: 1. Control of the chemical condition- ing process consists of maintain- ing an FeCI3 dose in the range of 6% to 12% (based on dry sludge solids) and adding sufficient lime to maintain a pH of 12.0. 2. The vacuum filter yield (wet weight/time) is controlled by ad- justing the drum speed. Vat level is adjusted to maintain a cake thick enough to discharge properly. Level is maintained by varying raw sludge flow rate, which in turn varies the chemical feed rates. 3. The hearth temperatures are ap- proximately 540°C (1000°F) on No. 2 and 950°C (1750°F) on No. 4. Temperature is controlled by ma- nipulating the burners on hearth Nos. 3 and 5, respectively. Furnace pressure is maintained at -0.38 to -0.51 cm (-0.15 to -0.20 in.) by manipulating the induced-draft fan damper. The flow of recycled cool- ing air is controlled to maintain a setpoint oxygen concentration in hearth No. 1. Additional air is gen- erally not required. The following is a summary of the performance of the sensors used during this study: Table 3. Recommended Temperature Profile for Controlled Incineration Temperature, °C (°F) Hearth No. 1 2 3 4 5 6 7 Minimum 400 (750) 450 (850) 650 (1200) 760 (1400) 590(1100) 200 (400) 80 (180) Average 430 (800) 480 (900) 700 (1300) 870 (1600) 650 (1200) 260 (500) 90 (200) Maximum 450 (850) 540 (1000) 760 (1400) 980 (1800) 700 (1300) 310 (600) 90 (200) Table 4. Dewatering Performance During Test No. 2 Parameter Hours Sludge flow, Us (gpm) Raw sludge solids, % FeC/a, % CaO, % Yield, wet mt/hr (TPH) Cake solids, % Cake volatile solids, % Process Train No. 1 (Computer) 11 4.4 (70) 4.1 11 18 4.7 20.5 53.8 Process Train No. 2 (Manual) 11 4.2 (66) 4.1 8.5 25 4.4 (4.9) 21.2 44.1 Parameter Hours Gas use, sm3/hr (SCFH) Gas use, sm3/wet mt (SCF/wet ton) Gas use, sm3/dry mt (SCF/dry ton) Total energy, kJ/kg H^ (BTU/lb H2O) Gas, kJ/kg H2O (BTU/lb H£» Process Train No. 1 (Computer) 11 184 (6,500) 39 (1,250) 184 (5,900) 4,885(2,100) 1,860 (800) Process Train No. 2 (Manual) 11 218 (7,700) 50 (1,600) 240 (7,700) 4,885(2,100) 2,325 (1,000) Acceptable Vat level Temperature Rotational speed Rotational position Sludge flow pH Solids Vacuum Cake weight Questionable ORP Oxygen Turbidity Unacceptable Viscosity Cake thickness Cake moisture Tank level sorship of the U.S. Environmental Pro- tection Agency. Several studies were conducted at Seneca to determine whether commer- cially available sensors could provide a continuous measure of cake moisture. All those tested were unacceptable, as they failed to provide reliable estimates of cake moisture. Even acceptable sensors require sig- nificant maintenance. The extreme is the conditioned sludge pH sensor, which required cleaning at least once per shift. Although the maintenance re- quired for the other sensors was lower. both the raw sludge solids sensor and the belt scale require frequent calibra- tion to assure success of the control system. Control of sludge-handling processes should be designed to allow operator- entered setpoints to maintain operation without going to complete manual operation. The full report was submitted in fulfill- ment of Grant No. S803602 by the Metropolitan Waste Control Commis- sion of St. Paul, Minnesota, under spon- •&U. S. GOVERNMENT PRINTING OFFICE:!986/646-116/20775 ------- R, C. Polta and D. A. Stulc are with the Metropolitan Waste Control Commission, St. Paul. MN 55101; and G. A. Mathes is with EMA, Inc., St. Paul. MM 55101. Waiter W. Schuk is the EPA Project Officer (see below). The complete report, entitled "Automation of Sludge Processing: Conditioning, Dewatering, and Incineration," (Order No. PB 86-138 963/AS; Cost: $22.95. subject to change) will be available only from: National Technical Information Service 5285 Port Royal Road Springfield, VA2216J Telephone: 703-487-4650 The EPA Project Officer can be contacted at: Water Engineering Research Laboratory U.S. Environmental Protection Agency Cincinnati. OH 45268 United States Environmental Protection Agency Center for Environmental Research Information Cincinnati OH 45268 BULK RATE POSTAGE & FEES PAID EPA PERMIT No. G-35 Official Business Penalty for Private Use $300 EPA/600/S2-85/140 LCD W TILLEY REGION V EPA LIBRARIAN 230 S DEAR30RN CHICAGO ST IL 60604 ------- |