United States Environmental Protection Agency Industrial Environmental Research Laboratory Research Triangle Park NC 27711 Research and Development EPA-600/S7-84-045 May 1984 Project Summary Pilot-Scale Parametric Testing of Spray Dryer S02 Scrubber for Low-to-Moderate Sulfur Coal Utility Applications N.J. Stevens, G.B. Manavizadeh, G.W. Taylor, and M.J. Widico A comprehensive dry SO, scrubbing test program was conducted which in- volved an in-depth field pilot study at the Comanche Station of Public Service Company of Colorado. The program in- vestigated the effects of a number of process variables on SO, removal. The ranges of process variables tested dur- ing the program were: inlet flue gas SO, concentration, 185-2150 ppm; stoichio- metric ratio, 0.5-6.4 moles lime/mole SO,; recycle ratio, 0-4.3 Ib* recycle solids/lb fresh lime; inlet flue gas temperature, 226-340°F; spray dryer flue gas outlet temperature, 128-210°F; and fabric filter temperature, 117-200°F. In the spray dryer, stoichiometric ratio, flue gas temperature approach to adiabatic saturation, and temperature drop across the spray dryer significantly influenced SO, removal. In the fabric filter, stoichiometric ratio and tempera- ture approach to adiabatic saturation controlled SO, removal. Recycling of flue gas desulfurization (FGD)/flyash product solids enhanced SO, removal over that of lime-only once-through operation. In the absence of fresh lime, recycle solids, and flyash solids in separate tests each produced about 20 percent SO, removal at a stoichiometry of 1 mole alkali/mole SO,. Over the range investigated (30 to over 90 per- cent), SO, removal correlated well with the key spray dryer and fabric filter pro- cess parameters. 1 EPA policy is to express all measurements in Agency documents in metric units. This project summary uses English units to improve clarity of presentation. Con- version factors are provided at the end of this summary. The final phase of the field test pro- gram consisted of a continuous demon- stration of dry SO, scrubbing tech- nology. The 5-day continuous run demonstrated that the spray dryer/ fabric filter system can achieve the 70 percent SO, removal level required to meet the New Source Performance Standards for low sulfur coal. Pilot test results related to stoichio- metry, recycle ratio, and unit operating temperatures provided the basis for a technoeconomic evaluation that showed that a spray dryer SO, removal system is less costly than limestone wet FGD/particulate control systems (fabric filter/limestone scrubber, ESP/lime- stone scrubber) for coal sulfur levels up to about 1.5-1.8 wt percent. Dry SO, scrubbing solid waste char- acteristics also were evaluated. Spray dryer product solids are coarser than fabric filter solids (30-35 \an versus about 10 urn mean diameter). Product solids chemical compositions from the two sources are similar, but spray dryer solids contain higher concentrations of unused reagent and fabric filter solids contain increased percentages of FGD products. Curing for 1 month at 72°F and about 100 percent relative humidity in- creased the cohesive strength of the waste solids by a factor of 3-6. Product solids leachate heavy metal contents are significantly less than hazardous waste maximum allowable levels. This Project Summary was developed by EPA's Industrial Environmental Re- search Laboratory, Research Triangle Park, NC, to announce key findings of ------- the research project that is fully documented in a separate report of the same title (see Project Report ordering information at back). Introduction Dry S02 scrubbing has emerged as a new technology and appears to be a cost- effective desulfurization process for low- sulfur western coals. Contracts for at least 10 first generation dry scrubbing systems already have been awarded, and many addi- tional projects are being evaluated. The at- tractiveness of the dry S02 scrubbing system compared to wet FGD lies in its physical simplicity, moderate pressure drop, very low water use, reduced reheat requirements, and the dry condition of the reduced volume of waste solids produced. The first example in the U.S. of dry S02 scrubber testing using a spray dryer for utility coal-fired boiler application occurred in the early 1970s. A spray dryer was used to remove S02 with an aqueous sodium car- bonate reagent. However, major spray dryer S02 scrubbing test activity began only as recently as 1977. At this time, several com- panies participated in spray drying and baghouse pilot testing at the Leland Olds Station of Basic Electric Power Cooperative. Sodium reagents were tested initially, but potential disposal problems and high costs turned the investigations toward other alkaline compounds. Additional testing in- dicated that slaked lime held the most pro- mise as an economical reagent for dry SO2 scrubbing. Pilot tests at the Hoot Lake Station of Otter Tail Power Company demonstrated greater than 90 percent overall S02 removal at a stoichiometric ratio of: 2.0-3.0 moles lime/mole SO2, using lime-only operation; and 1.0-1.5 moles lime/mole S02, with re- cycle. The study also identified the impor- tance of operating the spray dryer near the adiabatic saturation temperature to enhance S02 removal. The Hoot Lake results also showed that an alkaline flyash, especially under recycle operation, contributes significantly to S02 removal. Field and laboratory pilot tests utilizing a horizontal flow reactor and dual fluid atomization identified several variables that affect S02 removal. They include stoichio- metry, approach to adiabatic saturation temperature, inlet gas temperature to the system, and flyash alkalinity. Lime stoichio- metry was the primary correlating variable with S02 removal, but flyash alkalinity also played a strong role. S02 removal using flyash alone was 15-65 percent with highly alkaline Laramie River flyash. In 1981-82, parametric pilot tests at the Martin Drake Station of the City of Colorado Springs showed the importance of operating near the adiabatic saturation temperature on S02 removal, but found that in|et gas tem- perature to the spray dryer had a negligible effect. Using lime-only operation, S02 removal was considerably reduced at 2000 and 2500 ppm inlet S02 concentrations from that at 1000 and 1500 ppm S02. Fabric filter S02 removal in the Martin Drake tests was strongly affected by the approach to adiabatic saturation temperature and was also a function of stoichiometric ratio. The present program examines the sys- tematic application of dry SO2 scrubbing technology to treat utility flue gas using a spray dryer and fabric filter. A pilot test pro- gram at the Comanche Station of Public Ser- vice Company of Colorado investigates the effect of key process variables and recycled solids on S02 removal. Study of the fabric filter variables on S02 removal is confined to the effects that occur simultaneously with the testing of the spray dryer. Also, the pre- sent investigation does not address the effi- ciency of particulate removal in the dry scrubbing system. The final phase of the field test program is a continuous demonstration of spray dryer/fabric filter technology. The demonstration run is to verify that S02 removal can be achieved on a sustained basis to meet the New Source Performance Stan- dards (NSPS) for utility boilers operating on flue gas generated from low sulfur fuels. Field test results are utilized in a techno- economic evaluation to establish the areas where dry FGD technology may be applied economically. The characteristics of the solid wastes pro- duced from the dry S02 scrubbing system Bypass are also evaluated. Materials generated at the pilot test site are examined at the CES laboratory facilities. This limited scope pro- gram of testing and evaluation is to deter- mine 1} the basic composition of the waste products, and 2) the soil-mechanical and leaching properties of the FGD solids/flyash mixtures, to determine their suitability for landfill disposal or reuse. Solid samples are also analyzed for trace heavy metals to pro- vide hazardous waste information. Pilot System Description The pilot test system, Figure 1, is designed to treat up to 10,000 acfm (nominal) of flue gas. The system consists of a spray dryer to remove S02 followed by a fabric filter to col- lect dry FGD solids and flyash. An induced draft fan moves the flue gas through the system and a second "reverse air" fan is used to clean the fabric filter. Feed tanks and metering pumps supply reagent to the system. An S02 tank and delivery system provide additional SO2 to the flue gas for tests at higher inlet flue gas S02 concen- trations. Spray Dryer The pilot spray dryer is 8 ft in diameter, 35 ft high, and equipped with a variable- speed rotary-disc atomizer. The atomizer used in this program has a titanium body disc with silicon carbide ports around the periphery. The bottom plate of the disc is coated with aluminum oxide for protection against slurry abrasion. Dirty flue gas containng S02 and flyash enters the top of the spray dryer where it is intimately contacted with finely atomized lime slurry. The intimate contact and large Bypass Fabric Filter Compartments I SOi Injection Reagent Preparation Figure 1. Dry SOt scrubbing pilot flow schematic. \ / \ ml H J. "^ A JL | | | | j | I.D. Fan Stack —I > U To Ash Disposal ------- interfacial area of the spray dryer result in very rapid S02 absorption by the lime slurry. Most of the S02 removal in the overall system occurs in the spray dryer. Before leaving the dryer, the solids approach com- plete dryness. In the pilot unit, coarse solids settle in the conical bottom of the dryer and are discharged through a rotary valve to receiving drums. The scrubbed flue gas con- taining finer particles leaves the dryer through a side port and flows to the fabric filter. Fabric Filter The fabric filter is 10 x 15 x 55 ft and is operated with two compartments each designed to process about 5,000 cf m of flue gas. Commercial Teflon-coated fiberglass bags were used in the fabric filter. Each fabric filter bag is 12 in. in diameter, 30 ft high, and contains about 94 ft2 of bag sur- face. Twenty to 24 bags (10 to 12 per com- partment) were used in various tests during the pilot program. In the fabric filter, flyash and FGD solid paniculate are removed from the flue gas and additional S02 is removed. From the fabric filter, the flue gas flows to the induced draft fan and then to the stack. Flue gas from the spray dryer continuously enters the bot- tom of the fabric filter unit and leaves from the top. To limit pressure drop across the filter bags from the accumulation of collected solids, a flow of air periodically is passed through the bags in the reverse direction for a short period of time (1 to 2 min/hr). The "reverse air" flow dislodges most of the deposited solids from the bag surface; they drop into the collection hoppers, from where they are discharged through rotary valves. During the brief bag cleaning period, flue gas is bypassed around the fabric filter. Valves are operated from the control room either manually or automatically. Pilot Test Program The pilot test program consists of process variable parametric studies and two con- tinuous process demonstration runs (one short- and the other long-term). Process Variable Tests The process variable tests were empirical investigations designed primarily to identify the dominant variables that affect SO2 removal and to establish their relative impor- tance, rather than to determine why they are important or the underlying mechanisms in- volved. The parametric studies were carried out using two operating modes: (1) process variable tests using lime reagent in once- through operation with no product solids recycle; and (2) process variable tests incor- porating recycled solids. The process variables considered relevant to S02 removal were studied over the ranges of conditions shown in Table 1. Short-Term Process Demonstration A continuous process demonstration run was conducted to verify that S02 removal levels can be achieved on a sustained basis to meet New Source Performance Stan- dards. Specific operating conditions for the demonstration were selected, based on results of the process variable tests. Dry scrubbing system operability and control as well as S02 performance were observed over the course of the run. Conclusions of Major Process Variable Studies Spray Dryer S02 Removal 1. Parameters that dominate spray dryer S02 removal performance are: stoichio- metric ratio, SR; approach to adiabatic saturation temperature, ATAS/SD: temperature drop across the spray dryer, ATSO; and recycle ratio, RR. 2. Spray dryer S02 removal increases directly with fresh lime stoichiometry. At lower stoichiometries, SO2 removal in the spray dryer is quite sensitive to stoichiometric ratio. At higher stoichio- metries, S02 removal levels off and stoichiometric ratio has much less ef- fect on spray dryer S02 removal. 3. S02 removal efficiency in the spray dryer increases as the flue gas temper- ature approaches the adiabatic satura- tion temperature. 4. S02 removal in the spray dryer in- creases as the temperature drop across the spray dryer is increased. Spray dryer temperature drop directly reflects the liquid-to-gas ratio and the quantity of water fed to the dryer. 5. Spray dryer solids moisture content in- creases as the flue gas temperature ap- Table 1. Range of Pilot Test Variables Variable proaches the adiabatic saturation temperature. 6. The optimum spray dryer operating temperature strikes a balance between high SO2 removal and smooth trouble- free discharge and handling of moisture-laden product solids. 7. Spray dryer S02 removal is enhanced as the amount of recycle material (re- cycle ratio) increases. S02 removal in- creases as recycle ratio increases up to a value of about 2.5 Ib recycle solids/Ib fresh lime, where it levels off, indicating no further benefit to recycling additional solids. 8. Spray dryer flue gas residence time of 8-16 sec and spray dryer inlet S02 con- centration of 185-2150 ppm have very little effect on S02 removal. Fabric Filter S02 Removal I.The process parameters that significantly affect fabric filter S02 removal are: stoichiometric ratio, ap- proach to adiabatic saturation temper- ature, and recycle ratio. 2. S02 removal in the fabric filter increases proportionately with increasing fresh lime stoichiometry. 3. S02 removal in the fabric filter increases as the flue gas temperature approaches the adiabatic saturation temperature. 4. Product solids recycle enhances S02 removal across the fabric filter. 5. Air-to-cloth ratio and fabric filter inlet S02 concentration have negligible ef- fects on SO2 removal in the fabric filter. Overall S02 Removal 1. The dry scrubbing system can attain the 70-90 percent (see main report) S02 removal required by the New Source Performance Standards (NSPS). Lime stoichiometry is minimized by operating with recycle at high flue gas inlet temperature to the spray dryer, low spray dryer outlet temperature, and low fabric filter inlet temperature. Minimum Maximum Stoichiometric Ratio, moles CalOHh/mole SO2 in SO Met Flue Gas Temperature, °F SO Outlet Flue Gas Temperature, °F Fabric Filter Gas Temperature, °F Inlet SO2 Concentration, ppmv Atomizer Disc Diameter, in. Atomizer Disc Speed, rpm Inlet Flue Gas Rate, acfm Fabric Filter Air-to-C/oth Ratio, ft/min. Lime Slurry Feed Concentration, wt % Recycle Slurry Solids Concentration, wt % Recycle Ratio, Ib recycle solids/lb fresh lime 0.5 226 128 117 185 7% 10,600 3,000 1.3 3 10 0 6.4 340 210 200 2, ISO 8% 13,920 7,500 2.8 25 53 4.3 ------- 2. The spray dryer is the primary S02 con- trol unit in the system. The fabric filter is the primary participate control unit. In the present study, more than 75 per- cent of the total S02 was removed in the spray dryer, and considerably more than half of the total solids were col- lected in the fabric filter. Long-Term Process Demonstration A 5-day, 120-hour, continuous process demonstration run was successfully con- ducted without interruption and with negligi- ble operating problems. The continuous run demonstrated that the spray dryer/fabric filter system can achieve the 70 percent S02 removal level required to meet the New Source Performance Stan- dards for low sulfur coal (Figure 2). Waste Characterization Studies As part of the dry S02 scrubbing test pro- gram, a brief study was undertaken to char- acterize the solids wastes produced by the spray dryer/fabric filter dry scrubbing pro- cess. Only a modest amount of information has been published at the present time on the nature of the waste solids or their disposal characteristics. The FGD solids/flyash samples were col- lected at the Comanche test site during the pilot runs and sent to CES laboratory facilities for the characterization. To generate the samples, the pilot unit was operated steady-state at carefully chosen levels of stoichiometry and atomization until about 100 Ib of representative waste was collected. A wide spectrum of operating conditions is represented in the runs sampled. The operating conditions for each run in which samples were taken are summarized in Table 2. In most cases, a blend of 70 percent baghouse solids and 30 percent spray dryer solids (by weight) was tested. The 70/30 split is normal for typical operating conditions, such as those given in Table 3. In three cases, only fabric filter solids were tested; in one other run, only spray dryer solids were evaluated. Conclusions of Waste Characterization 1. Optimum compacted densities of 78-90 Ib/ft3 are obtained at dry waste solids moisture contents of 25-35 wt percent H20. Dry scrubbing waste product compacted densities are lower, and cor- responding moisture contents are higher than values reported for sludge/flyash blends from wet FGD systems (115-120 Ib/ft3 and 15-20 wt percent H20). 2. The cohesive strength and angle of in- ternal friction of waste products from the lime-only runs are 40-50 percent greater than for the waste products from recycle runs. Cohesive strength in- creases 3- to 10-fold and angle of in- ternal friction increases 30-50 percent upon curing of waste solids for approx- imately 1 month at 72 °F and about 100 percent relative humidity (Table 3). 3. Permeability values for uncured dry scrubbing product solids are of the order of 10"5 cm/sec. For samples cured approximately 1 month at 72°F and 100 percent relative humidity, permeability is 10-MO-7 cm/sec (Table 3). 4. The total dissolved solids content of the leachate from the dry scrubbing waste products generally exceeds 1200 ppm; most of it is attributable to CaS04. Technoeconomic Study A technoeconomic study was performed to compare a dry S02 scrubbing system us- ing lime reagent with wet FGD systems us- ing limestone. The S02/particulate pollution control systems evaluated in this study in- 12/12/80 12/13/80 12/14/80 12/15/80 12/16/80 ffU 7n eo S "5 O 1 40 Overall SOi 1 8 20 1O > 1 1 f • Target Value * 1 * 0lr • • » , • q • Overall % SOz Removal - • • • 1 1 1 1 1 1 1 l • Test Conditions SOz IN = 480-520 ppm AT — OC OJ7OC **' AS/SD *• -tO-oO r ArAS/FF=45-55°/: Overall Stoichiometric Ratic \ i 1 . "*" - - f. - 1 to 20 30 40 50 60 70 Elapsed Time, hr 80 90 100 110 120 130 Figure 2. Process demonstration test results—overall SO2 removal and overall Stoichiometric ratio. 4 O to •8 I I Q 5 .e> I . I 5 to ------- eluded: a spray dryer followed by a fabric filter {SD/FF), a fabric filter followed by a single-loop wet scrubber (FF/LS), and an electrostatic precipitatof followed by a single- loop wet scrubber (ESP/LS). Capital investment and annual operating costs were estimated and compared for the three pollution control systems studied. In addition, sensitivity analysis clarified the ef- fect of system size (MW) and percent S in the coal on unit capital and unit operating costs. The effects of percent S in the coal and reagent price on lime reagent costs were also determined. Study Design Basis For the technoeconomic studies, a power plant in Colorado was used as the basis since the pilot test work was performed at the Comanche Station of Public Service of Col- orado in Pueblo. The Powder River Basin coal used in this study had a heating value of 8230 Btu/lb and contained 0.6 percent sulfur, 5.77 percent ash, and 30.5 percent water. The S02 and particulate removal ef- ficiencies were based on New Source Per- formance Standards of 0.6 Ib SOz/106 Btu and 0.03 Ib particulate/108 Btu. The system design basis specified for these conditions is presented in Table 4. Economic Basis The technoeconomic comparisons were based on estimates of capital and operating costs for the three S02/particulate control systems. Capital costs include direct, in- direct, and contingency costs, but not such charges as allowance for system start-up and modification, interest for system construc- tion, land, working capital, and royalties. The capital cost estimates for the spray dryer, fabric filter, and electrostatic precipitator are based on Research-Cottrell cost estimate in- formation. Capital cost estimates for the limestone scrubber are based on TVA values. Operating costs, including direct and indirect costs, are presented as first-year annual revenue requirements. Capital and operating cost estimates are calculated based on first- quarter 1981 dollars. Equipment included in each pollution con- trol system was divided into functional areas for cost estimating purposes. The direct cost of each area was estimated independently. The total direct investment for each system is the sum of the six process area direct costs. Indirect investment was assumed to be 30 percent of the total direct system in- vestment. Contingency costs were of the sum of direct and indirect costs. Capital Cost Estimates Comparison of the total capital investment costs for the three S02/particulate pollution control systems shows that the dry scrub- bing system is less costly than the two wet FGD systems. Table 5 shows that the total capital investment for a 500 NW spray dryer/fabric filter system treating flue gas generated from 0.6 percent S coal is Table 2. Operating Conditions for Pilot Plant Runs Chosen for Waste Characterization Sampling Run No. 220 314 317 405R2 506 624 923 923 923 Sample Source Blend Blend Blend Fabric Filter Fabric Filter Blend Spray Dryer Fabric Filter Blend Inlet Concen- tration ppmv 1350 1900 2150 760 850 780 1380 1380 1380 Over- all *?o OV2 Re- moval % 39.4 37.1 43.1 59.3 50.9 39.9 72.2 72.2 72.2 Stoichio- Ratio moles lime/ moles SOt in 3.01 2.16 1.05 1.07 2.01 1.04 1.14 1.14 1.14 Recycle Ratio Ib recycle solids/lb makeup lime 0 0 0 2.27 0 1.06 2.62 2.62 2.62 Spray Dryer Tempera- ture In- let °F 268 264 345 340 258 295 255 255 255 Out- let °F 188 183 185 180 178 177 147 147 147 hTAS/SD °F 71 68 70 50 48 48 22 22 22 Spray Dryer Resi- dence Time sec 10.0 10.2 10.4 10.2 9.5 9.9 9.4 9.4 9.4 Table 3. Product So/ids Triaxial Compression and Permeability Test Results Uncured Cured3 Permeability Run No. 220 314 317 405-R2 BOB 624 923 923 923 Operation Mode Lime-Only Lime-Only Lime-Only Recycle Lime-Only Recycle Recycle Recycle Recycle Sample Source Blend* Blend Blend Fabric Filter Fabric Filter Blend Spray Dryer Fabric Filter Blend Cohesion psi 16.3 18.2 15.8 6.0 14.0 13.0 12.0 12.1 J0.2 Angle of Internal Friction degrees 36 39 37 33 34 32.5 24 21 22 Cohesion psi 110 _ 63 63 34 — _ - Angle of Internal Friction degrees 51 _ 51 48.5 42 _ _ - Uncured cm/sec 0.3 x 10-* 0.4 x 10-* 1.2 x 10-* 0.2 x 1fr* 3.3 x 10-* 8.9 x 10-* 7. 1 x 10-* 9.3 x 70-6 5.3 x 10-* Cured cm/sec 3.5 x 70-«c _ 3.5 x 10+d 0.7 x 10** 0.9 x 10** — - 8 Cured for 28 days at 72°F and about 100 percent relative humidity. b Blend refers to a physical mixture of 70 wt percent fabric filter solids and 30 wt percent spray dryer solids. c Cured for 35 days at 72°F and about 100 percent relative humidity. d Cured for 38 days at 72°F and about 100 percent relative humdity. ------- estimated at $42,300,000. The fabric filter/ limestone scrubber system cost estimate is $59,046,000. The ESP/limestone scrubber system cost estimate is $63,699,000. The conclusions on capital investment reached during the study are similar to those presented by a TVA study. In each study, the total fixed capital investment for the dry scrubbing system is about 30 percent less than for an ESP/limestone scrubber system. However, the fixed capital investment figures developed in the present study are 15-20 per- cent less than the corresponding TVA estimates. A significant part of the difference arises because the capital investment esti- mates of the present study are based on ac- tual first-quarter 1981 dollars while the TVA study uses projected mid-1982 dollars. In view of the ±30 percent error range associated with study or preliminary esti- mates, the capital investment costs generated for these and the TVA evaluations agree fairly well. These cost estimates show that dry system costs are 30-35 percent lower than wet FGD/particulate systems costs for low sulfur coal applications. Unit costs for the three systems at a 500 MW size are $84.6/kW for the spray dryer/fabric filter, $118.1/kW for the fabric filter/limestone scrubber, and $127.4/kW for the ESP/limestone scrubber case. Operating Cost Estimates Annual operating costs (first-year annual revenues) were estimated for the three pollu- tion control cases for a 500 MW power plant burning 0.6 wt percent S coal and operating 7000 hr/yr. Cost comparisons in Table 6 show that dry scrubbing system operating costs are about 25-30 percent lower than wet FGD/particulate control systems costs under the conditions investigated. All operating cost items except raw materials, or reagent, costs are less for the dry scrubber system. Reagent costs are much higher for dry scrub- bing than for wet scrubbing primarily because of the large cost differential be- tween lime and limestone, $70 vs. $8/ton. Essentially all of the operating cost difference between dry and wet scrubbing systems determined in the present study is at- tributable to capital investment-related items, maintenance, and capital charges. The results of the present study and those of TVA indicate that dry scrubbing annual operating costs are 25-30 percent less than ESP/limestone scrubber costs. Annual operating cost estimates of this study are only 70-75 percent of those developed by TVA. Much of the annual operating cost dif- ference is attributable to lower capital charges used in the present study compared to the TVA work. Lower operating labor Table 4. Study Design Basis Item Design Value Flue Gas Rate, acfm SO2 Met Concentration, ppm Flue Gas Inlet Temperature, °F Atmospheric Pressure, psi SO2 Removal Efficiency, % Paniculate Inlet Content, gr/acf Particulate Removal Efficiency, % 2,040,000 600 275 12.3 70 2.3 99.7 Table S. Comparison of System Total Capita/ Investments (500 MW, 0.6% S Coal, 70% SOt Removal) Total Cost, 1000$ (1981$) Investment Area Material Hand/ing Feed Preparation Gas Hand/ing SO2 Absorption Particulate Removal Waste Disposal Total Direct Investment Indirect Investment Contingency Total Fixed Investment Unit Cost ($/kW) Lime Spray Dryer/ Fabric Filter 3,391 850 5,975 7,145 9,230 524 27,115 8,135 7,050 42,300 84.6 Fabric Filter/ Limestone Scrubber 800 1,100 8,554 11,802 10,990 4,604 37,850 11,355 9,841 59,046 118.1 Electrostatic Precipitator/ Limestone Scrubber 800 1,100 8,554 11,802 13,973 4,604 40,833 12,250 10,616 63,699 127.4 Table 6. Comparison of System Annual Operating Costs (500 MW, 0.6% S Coal, 70% S02 Removal, 7000hr/yr Operation) Total Cost, 1000$ 11981$) Item Raw Materials Electricity Water Maintenance Operating Labor Overhead Administration Capital Charges Total Cost, 1000$ Unit Cost, mil/s/kWh Lime Spray Dryer Fabric Filter 1,026 1,820 40 1.654 649 832 65 6,345 12,431 3.6 Fabric Filter/ Limestone Scrubber 225 2,282 73 3,217 774 1,269 77 8,857 16,774 4.8 Electrostatic Precipitator/ Limestone Scrubber 225 2,487 73 3,062 749 1,274 75 9,555 17,500 5.0 hourly rates and costs of this study also account for some of the operating cost difference. Lime Reagent Cost For the present study, lime reagent costs are somewhat more sensitive to increases in' the coal sulfur content than to raw material price. Lime costs increase 5-7 times to meet the reagent requirements as coal sulfur in- creases from 0.6 to 1.5 wt percent. In this coal sulfur range, lime reagent costs (at a price of $70/ton) increase from less than 10 percent of the total operating costs at 0.6 percent to about 30 percent at 1.5 percent S. Since lime reagent cost is very sensitive to sulfur level, dry scrubbing enjoys its greatest economic advantage over wet FGD systems for low sulfur coal applications. As coal sulfur content increases, the cost dif- ference between wet and dry systems de- creases. The operating cost crossover point is estimated at somewhat greater than 1.5 percent S coal for the bases used in the pre- sent study (Figure 3). Note that the spray dryer/fabric filter operating cost increases more rapidly as the coal sulfur content in- creases. This is due to the greater lime re- quirement (higher stoichiometric ratios) as the sulfur content increases. ------- I 5 « I Fabric Filter/Wet Scrubber (Limestone) ESP/Wet Scrubber (LSi Spray Dryer/Fabric Filter (Lime) 500 MW System 1981 $ 0.6 1.0 1.5 1.9 Percent S in Coal Figure 3. Unit operating cost sensitivity. Conclusions of Technoeconomic Study 1. The capital investment required for a dry S02 scrubbing system (spray dryer/ fabric filter) is 30-35 percent less than for either of the two wet FGD systems (fabric filter/limestone scrubber, ESP/ limestone scrubber) based on estimates for a 500 MW unit burning Powder River Basin coal with 0.6 percent sulfur and complying with the NSPS. 2. Annual operating costs (first year an- nual revenues) for a dry S02 scrubbing system (spray dryer/fabric filter) are 25-30 percent lower than for either wet scrubbing system (fabric filter/lime- stone scrubber, ESP/limestone scrubber). 3. Reagent costs for a dry scrubbing system using lime are much higher than for wet scrubbing systems using lime- stone. Lime costs 4-5 times as much as limestone for S02 control of flue gas generated from 0.6 wt percent sulfur coal and is a major operating expense for dry scrubbing systems. Lime reagent cost is affected by coal sulfur content, stoichiometric ratio, and raw materials price. 4. Unit capital costs are only moderately sensitive to system size (MW) for all three systems and increase as coal sulfur content increases (see main report). Dry scrubbing system costs are more sensitive to coal sulfur content than are wet scrubbing system costs. 5. For each of the three desulfurization processes, unit operating costs de- crease as system size (MW) increases but are not very sensitive to size. Unit operating costs increase as coal sulfur content increases because of increased reagent use. Dry scrubbing system operating costs are more sensitive to coal sulfur content than are wet scrub- bing system operating costs because dry systems use more-expensive lime as the reagent. 6. As coal sulfur content increases, the cost advantage of a dry system over a wet system decreases. The crossover range is about 1.5-1.8 percent sulfur for the conditions used in this study. Conversion Factors To Convert From English cfm ft gr/scf in. in. H2O Ib gal. gal./1000 ft3 Btu short ton °F To SI nWhr m kg/m3 m Pa kg m3 liters/m3 joule tonne °C Multiply By 1.70 0.305 0.00229 0.0254 249 0.454 3.79 0.13 0.252 0.91 5/9(°F-32) ------- N. J. Stevens, G. B. Manavizadeh, G. W. Taylor, and M. J. Widico are with Cottrell Environmental Sciences, Inc., Sommerville, NJ 08876. Theodore G. Brna is the EPA Project Officer (see below). The complete report, entitled "Pilot-Scale Parametric Testing of Spray Dryer S02 Scrubber for Low-to-Moderate Sulfur Coal Utility Applications," (Order No. PB 84-175 959; Cost: $22.00. subject to change) will be available only from: National Technical Information Service 5285 Port Royal Road Springfield, VA22161 Telephone: 703-487-4650 The EPA Project Officer can be contacted at: Industrial Environmental Research Laboratory U.S. Environmental Protection Agency Research Triangle Park, NC27711 United States Environmental Protection Agency Center for Environmental Research Information Cincinnati OH 45268 Official Business Penalty for Private Use S30O U.S. GOVERNMENT PRINTING OFFICE: 1984-759-102/0943 ------- |