United States
Environmental Protection
Agency
 Industrial Environmental Research
 Laboratory
 Research Triangle Park NC 27711
Research and Development
 EPA-600/S7-84-065 July 1984
Project Summary
Results of the First 2 Years  of
Commercial  Operation  of  an
Organic-Acid-Enhanced  FGD
System

R. L Glover, G. E. Brown, J. C. Dickerman, and O. W. Hargrove
  The U.S. EPA has sponsored research
to develop organic-acid-enhanced flue
gas desulfurization (FGD) technology
for existing and new coal burning facil-
ities. A 1981 EPA-sponsored demon-
stration program at  Springfield  City
Utilities'  Southwest  Power Plant
(SWPP), near Springfield, MO, showed
that adipic acid and dibasic acid (DBA)
greatly enhanced FGD performance.
SWPP has continued to use DBA to
comply with the 1971 SO2 emissions
standard under which they are regulat-
ed.  Thus. SWPP became  the first
commercial-scale system to use an
organic additive to enhance SO2 remov-
al.
  This report documents the first 2
years (1982  and 1983) of commercial
operation of the DBA system at SWPP.
During 1982 and 1983, SWPP aver-
aged an SO2 emission rate of less than
1.0 Ib  SO2/106 Btu. Conversely, in
1980 (prior  to DBA  addition), SWPP
averaged about 5 Ib SO2/106 Btu. FGD
system reliability was also greatly im-
proved, averaging 97.9 percent in 1982
and 98.7 percent in 1983, compared to
45 percent in 1980. The SO2/O2 con-
tinuous emissions monitoring system
also exhibited excellent reliability, ex-
ceeding 97 percent. Overall, DBA has
increased the flexibility of the SWPP
system and, most importantly, allowed
SWPP to operate in compliance.

  This Project Summary was developed
by EPA's Industrial Environmental Re-
search Laboratory, Research Triangle
Park, NC, to announce key findings of
the research project that is fully docu-
mented in a separate report of the same
title (see Project Report ordering infor-
mation at back).

Introduction
  EPA's Industrial Environmental  Re-
search  Laboratory at Research Triangle
Park (IERL-RTP) has an ongoing research
and development program to improve the
performance of lime/limestone flue gas
desulfurization (FGD) systems. One of the
most promising aspects of that effort has
been the use of organic acids as buffering
agents  to increase soluble alkalinity in
limestone FGD systems. Adipic acid was
identified as a suitable additive because
of physical  properties,  availability, and
cost. After extensive laboratory-, pilot-,
and prototype-scale studies on adipic-
acid-enhanced limestone systems, EPA,
in 1981, sponsored a full-scale demon-
stration at SWPP.
  Nine months of testing was conducted
at SWPP. Four months were spent at the
beginning of the program investigating
adipic acid addition in a forced oxidation
system. Better than 90 percent SO2
removal was achieved in a 49-day run,
the longest continuous operating period
at SWPP at that time. Next, adipic acid
addition achieved 85 -  95 percent SO2
removal in  a  natural oxidation system
over a period of 3-1/2 months.
  Finally, a  mixture of organic dibasic
acids (DBA) was tested over  a 6-week
period following the adipic acid testing.
DBA, a  by-product of adipic acid manu-

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   facturing, contains adipic, glutaric, and
   succinic acids, and is less expensive than
   adipic acid. Testi ng at SWPP showed DBA
   to be very effective in enhancing FGD
   system performance, resulting in a signif-
   icant decrease in SO2 emissions.
     An analysis was then performed to
   determine the most cost-effective option
   which  would enable SWPP to  comply
   with the 1971  SO2 emissions standard.
   Options considered included increasing
   the slurry rate to the scrubbers, convert-
   ing the scrubbers to spray towers, adipic
   acid enhancement, and DBA addition.
   Lower costs associated with the DBA
   option, as well as its demonstrated effec-
   tiveness, led  SWPP to select DBA for
   long-term use. In doing so, SWPP became
   the first commercial-scale facility to utilize
   DBA in  an FGD system application. This
   report documents commercial operation
   of SWPP's DBA system, between January
   1982 and December 1983.
Program Objectives
  Since operation at SWPP represents
the first commercial scale use  of an
organic acid-enhanced FGD system, IERL-
RTP personnel decided it would be useful
to the  industry to document system
performance following the demonstration
program. Consequently, in  May  1982,
Radian  Corporation was contracted to
monitor S02 emissions and the overall
process conditions at SWPP. The primary
objectives of this program were to evalu-
ate the performance of the DBA-enhanced
system and to note any long-term effects
on the  process. A secondary objective
was to document the performance of the
continuous emissions monitoring  equip-
ment in 1982 to determine the ability of
that equipment to collect data as required
in the 1979 revisions to the utility NSPS.
A brief description  of the SWPP system
and a summary of the monitoring pro-
gram results are presented here.
FGD System Description
  The SWPP FGD system consists of two
parallel tray tower modules, each sized to
handle 60 percent of the design flow. The
coal typically contains 3.5 - 4.0 percent
sulfur, corresponding  to inlet flue gas
concentrations of 2000 - 2600 ppm SOz.
Limestone preparation, sludge dewater-
ing, and sludge disposal  systems are
common to the two modules.
  Figure 1 shows the overall flow scheme
for the FGD system. The flue gas enters
the presaturator, where it is cooled by
clarified  liquor  (supernatant) from the
thickener. The gas then passes through
three  levels of gas/liquid contact trays,
the mist eliminator, and out of the stack.
No flue gas reheat is used.
  Slurry is circulated from the reaction
tank below the  scrubber through spray
nozzles  above the top  level of  trays.
Makeup  limestone is added  from the
limestone storage tank to  the reaction
                                       Thickener
                                       Overflow
                                                                                                           Limestone
      Supernatant
   (Thickener Overflow)
    Return to Process
                                                           Vacuum
                                                            Filter
                                                                                        Sludge to
                                                                                         Landfill
   Figure  1.   SWPP FGD flow scheme.

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tank to maintain the pH set point. Solids
are first settled in the thickener, and the
thickener underflow slurry is dewatered
on  a vacuum  filter belt.  The resulting
sludge is mixed with fly ash in the pug mill
and trucked to an on-site landfill. Super-
natant (thickener  overflow) from the
dewatering operation is returned to the
FGD modules as presaturator and mist
eliminator wash water. Additional super-
natant water is utilized in the limestone
preparation area.
  A temporary DBA feed system was
installed to add DBA solution on a con-
tinuous basis. DBA is delivered on site in
6000 gal.  (22,710 liter) tank trucks. Hot
water (~140°F,  60°C) was circulated
through a steam jacket surrounding the
tank to inhibit DBA crystallization.
  Initially, DBA was pumped from the
tank truck to the ball mill sump. The feed
rate was set manually. After the DBA was
mixed with the freshly ground limestone
slurry from the ball mills, the mixture was
pumped to the limestone storage  tank.
Since the limestone handling equipment
was common to both scrubber modules,
both  scrubbers operated  at essentially
the same DBA concentration. Later (in
September 1982), the DBA feed system
was modified  to allow DBA to be fed
separately into the reaction tank of either
scrubber.
  In May  1983, SWPP began operating
with  a  permanent DBA  feed system,
including  an 18,000 gal. (68,000  liter)
stainless steel storage tank, an immersion
heater, two 30-gpm(114liters/min)DBA
circulation  pumps,  feed lines to the
individual  modules, and a  source of
heated flush water. SWPP estimates the
cost of the permanent system at approxi-
mately $300,000.  To date, SWPP has
reported no problems with the permanent
feed system.


Program Results
  Analysis of the  SWPP FGD system
operation in 1982 and 1983 shows that
the DBA-enhanced  system is continuing
to perform well. SO2 emissions averaged
less than 1.0 Ib SO2/106 Btu (430 ng/J)
in 1982 and 1983, compared to about 5 Ib
SO2/106 Btu (2170 ng/J) in 1980 (before
DBA use). FGD system reliability averaged
nearly 98 percent in 1982 and almost 99
percent in 1983, compared to 45 percent
in 1980, before the adipic acid demon-
stration program.
  The flexibility of the DBA-enhanced
system was well  demonstrated in  1982
as SWPP personnel adjusted conditions
to minimize scaling in the mist eliminators
before installing limestone classifiers.
The pH set point was reduced, from the
5.4 used during the DBA demonstration,
to 5.0. The reduced pH resulted in in-
creased limestone utilization which
helped maintain mist eliminator reliabil-
ity. Higher DBA concentrations were
required with the lower pH setting, which
resulted in a  higher DBA consumption
rate; i.e., 30 Ib DBA/ton S02 (15 g/kg
S02) removed compared to 15 Ib/ton (25
g/kg) in the demonstration program. How-
ever, system reliability was maintained at
a very  high  level in spite  of  a poor
limestone grind. The installation of lime-
stone classifiers in late 1982 permits
operation at higher pH with good lime-
stone utilization. 1983 results reported by
SWPP show that DBA consumption was
reduced to about 25 Ib per ton S0z(5 g/kg
S02) using the new classifier system.
Further reduction  in DBA consumption
may be possible.
  Finally, the continuous emissions mon-
itoring (CEM) system performed  very
well. Although  called upon to operate
nearly all of 1982 (except  for boiler
outages in April and December), average
system reliability was 97 percent. Only
minor problems were experienced, most
of which involved power interruptions to
the DART® microprocessor. During 1983,
very few problems were noted with the
CEM system.

Conclusions
  SWPP's FGD system continues to per-
form very well with  respect  to both
reliability and S02 reductions. DBA  has
increased the  versatility  of the FGD
system as shown by the successful
operation at pH 5.0. SO2 emissions were
well within the 1.2 Ib S02/106 Btu (520
ng/J) limit, and the reliability of both the
FGD system and the CEM system through-
out 1982 and 1983 were excellent. The
following conclusions can be drawn from
this program:
• Use of DBA allows SWPP to remain in
   compliance with the S02 regulation.
   An average S02 emission of less than
   1.0 Ib SO2/106 Btu (430 ng/J) was
   measured in 1982 and 1983 with DBA
   addition compared to 5 Ib SO2/106 Btu
   (2170 ng/J) in 1980, before the adipic
   acid demonstration program.
• DBA greatly increases the flexibility of
   the FGD system, allowing successful
   operation over a wide pH range. Opera-
   tion at a reduced pH, in conjunction
   with better utilization of fresh water to
   the  FGD system, allowed SWPP to
   achieve an overall reliability of 97.9
  percent in 1982, and 98.7 percent in
  1983.
• Limestone classification and grinding
  circuit performance is important  to
  overall system performance. In 1982,
  DBA consumption at SWPP was about
  30  Ib/ton S02 (15 g/kg SO?), due
  primarily to operating at a lower pH
  and a decrease in recycle pump per-
  formance. A limestone classification
  system  was installed in  late 1982,
  enabling the system to operate at a pH
  of 5.6-5.8 with good limestone utiliza-
  tion. Higher pH operation reduced the
  DBA consumption  rate to about 25
  Ib/ton S02 (5  g/kg S02) in 1983.
  Further reductions  in DBA consump-
  tion may be possible.
• Finally, CEM systems can be reliable in
  commercial operation. The CEM sys-
  tem at SWPP was 97 percent reliable
  during 1982. The  relative accuracy
  remained well within tolerance limits
  set by EPA. Based on these results, the
  CEM system can reliably and accurate-
  ly supply the data necessary to com-
  pute 30-day rolling average emission
  rates over a long period.

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    R. Glover, G. Brown, J. Dickerman, and 0. Hargrove are with Radian Corp., A ustin,
      TX 78759.
    J. David Mobley is the EPA Project Officer (see below).
    The complete report, entitled "Results  of the First 2 Years of Commercial
      Operation of an Organic-Acid-Enhanced FGD System," {Order No. PB 84-207
      679; Cost: $10.00, subject to change) will be available only from:
            National Technical Information Service
            5285 Port Royal Road
            Springfield,  VA 22161
            Telephone: 703-487-4650
    The EPA Project Officer can be contacted at:
            Industrial Environmental Research Laboratory
            U.S. Environmental Protection Agency
            Research Triangle Park, NC 27711
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