United States
                    Environmental Protection
                    Agency
Industrial Environmental
Research Laboratory
Research Triangle Park NC 27711
                    Research and Development
EPA-600/S7-84-079 Sept. 1984
&ER&         Project  Summary
                    Evaluation  of Long-Term  NOX
                    Reduction  on  Pulverized-Coal-
                    Fired Steam  Generators
                    S.S. Cherry
                      Long-term NO, emission data from
                    eight pulverized-coal-fired steam gen-
                    erators were analyzed for the purpose
                    of quantifying the effectiveness of
                    various combustion modifications. All
                    boilers,  but one,  were modified to
                    reduce NO* emissions. These combus-
                    tion modifications included changing
                    both hardware and operating procedures.
                    All boilers were subject to the NO* pro-
                    visions  of the  1971  New  Source
                    Performance Standards  (NSPS).
                      In several instances, when long-term
                    emission data for the period before the
                    modification were not  available, the
                    quantification of the NO, reduction was
                    based on the result of the performance
                    test required by the 1971 NSPS. NO,
                    reductions of from 5.1  to 60 percent
                    were determined without incurring sig-
                    nificant adverse impacts on unit opera-
                    tion. NO, emission levels, determined
                    from the performance tests, were from
                    146 to 473 ng/J (0.34 to 1.10 lb/106
                    Btu) before control implementation and
                    from 148 to 281 ng/J  (0.34 to 0.65
                    lb/106 Btu) after combustion modifica-
                    tions were applied.
                      This Project Summary was developed
                    by EPA's Industrial Environmental
                    Research Laboratory. Research Triangle
                    Park. NC. to announce key findings of
                    the research project that is fully docu-
                    mented in a separate report of the same
                    title (see Project Report ordering infor-
                    mation at back).

                    Introduction and Summary
                      Previous work in this program identi-
                    fied pulverized-coal-fired steam genera-
                    tors that had been  modified for the
                    express purpose of reducing NO, emis-
                    sions. These modifications included
changes of both hardware (e.g., burner
substitution) and operating procedures
(e.g., overfire air system adjustment).
  The  purpose  of this  work was to
quantify the NO reduction achieved by
comparing long-term (approximately 30
days) emission data obtained before and
after the modification. Whenever possible,
the  effect of the modification on unit
efficiency was also to be quantified. The
emission data was  to be obtained by
certified NO and 02 (or CO2) analyzers. In
addition, the unit load (in either gross
MWe or steam flow) and coal analyses
were requested  from the participating
organizations.
  Table-1  summarizes the eight steam
generators which were analyzed, the
modification(s) implemented, and the NO,
reduction  achieved at high load. Also
shown are the post-modification levels.
For several of these units, emission data
before the modification were not availa-
ble,  in which case the NO, reduction was
referenced to the result of the perform-
ance test required  by  the 1971 New
Source Performance Standards. (All units
were subject to the 1971 NSPS.) The two
NO, reduction values shown for Gentle-
man Unit  1 are due to the utility's
questioning of the initial performance
test results.
  Iowa Power and Light's Council Bluffs
Unit 3 is an exception in that the excess
air level was increased in an attempt to
reduce slagging. However,  the NO,
increase resulting from this operational
change was also interpreted in a bilateral
manner; i.e., as  a NO, decrease due to
lower excess air when the high 02 data
was used as a "before" condition.
  The  NO, reduction at other than high
load was also quantified when long-term

-------
Table 1 . Data Base and High-Load /VO« Reduction
Utility Station Unit
Iowa Power & Light
Utah Power & Light
Proprietary
Proprietary
Proprietary
Nebraska Public
Power District
Proprietary
Council Bluffs 3
Hunter 2
A
B
C
Gentleman 1
D
E
Boiler
Mfg.1*
B&W
CE
RS
RS
RS
FW
B&W
B&W
Coal
Type™
Sub
Bit
Bit
Bit
Bit
Sub
Bit
Bit
Gross
MWe
720
425
417
360
360
680
81.9""
81.9""
Modification™
LEA
LNCFS. OFAA
RB. UFA
RB
RB
OFAA. LEA
CO
CO
NO,
Reduction, %
5.1
39
40
40
41
49, 60
15
21
Post Mod.
NO
ng/J
148
155
269
279
245
188
281
236
131 B&W=Babcock & Wilcox
    CE=Combustion Engineering
    RS=Riley Stoker
    FW=Foster Wheeler

lb> Sub=Subbituminous
   Bit=Bituminous
{cl LEA -Lower excess air
LNCFS=Low-NOi concentric firing system
 OFAA -Overtire air adjustment
   RB=Reburnering
  UFA - Underfire air added
   CO = CO-based control
"" Rated steam flow, kg/s
emission data were available both before
and after  implementing combustion
modification.


Discussion
  The analysis is illustrated in Figures 1
and 2 for Iowa Power and Light, Council
Bluffs Unit 3.  Continuous emission
monitor (CEM) and load  data  were
supplied by the utility for two periods:
February 16 - May 29, 1981     low 02
                            operation
May 30 - July 15,  1982         high O2
                            operation
Figure  1  compares the NO  vs.  load
characteristic for both periods. This char-
acteristic was developed by  sorting the
hourly  averaged  NO into  10 equally
spaced load increments (cells) which
ranged from the minimum to the  maxi-
mum loads. (Not shown in Figure 1 are
the results for the two lowest load cells
for which insufficient data were available
to make a meaningful comparison.) The
NO* measured during the unit's perform-
ance test (as required by the 1971 NSPS)
is also shown for reference.
  An analysis was conducted to deter-
mine  if  the NO characteristics  were
statistically different with  the results
shown in Figure 2. In this instance, the
higher Oa during  1982  was used as a
"before" condition in order to quantify
the  NO reduction  resulting  from  lower
excess air operation. As noted, the NO
  175
  150
  125
  100
o
   75
   50
   25
                       \
              - 1981 (LowOi)
              -- 1982 (High OJ
                   Performance WO*
                      200
    400

Load, MWe (gross)
                                                        600
                                                                         500
Figure  1.    NO versus load comparison—Iowa Power and Light, Council Bluffs Unit 3.

-------
N o OB 
-------
United States
Environmental Protection
Agency
Center for Environmental Research
Information
Cincinnati OH 45268
Official Business
Penalty for Private Use $300

-------