United States
 Environmental Protection
 Agency
 Industrial Environmental Research
 Laboratory
 Research Triangle Park NC 2771
 Research and Development
 EPA-600/S7-82-057a  Mar. 198
 Project Summary
 Hitachi Zosen  NOX Flue  Gas
 Treatment  Process:
 Volume  1.  Pilot  Plant
 Evaluation
 Shingo Tanaka and Richard Wiener
  The EPA/Hitachi Zosen pilot plant
project — evaluating selective cataly-
tic reduction (SCR) of NOx on a coal-
fired source — operated for a year and
a half. The objective of the contract, to
operate at 90% NOx removal over a
90-day period, was exceeded. TheO.5
MW pilot plant was  installed on a
slipstream from Georgia  Power Co.'s
Plant Mitchell near Albany, GA.
  A newly developed catalyst, NOXNON
600, was successfully applied and
demonstrated  90%  NOx removal
efficiency for over 5600  hours. Tests
to operate the catalyst outside of
design specifications showed good
tolerance to adverse situations.
  The pilot plant project was the first
demonstration and evaluation of NOx
SCR technology  on a coal-fired
source in  the U.S. Project results
indicate  that the process may be
usable as a  NOx  control option;
however,  some technical concerns
remain before the technology can be
considered commercially available
and demonstrated for coal-fired sources
in the U.S.
  This Project Summary was devel-
oped by EPA's Industrial Environmen-
tal Research  Laboratory, Research
Triangle Park, NC, to announce key
findings of the research project that is
fully documented in a separate report
of the same title (see Project Report
ordering information at back).
 Introduction
  As part of the effort to  assess
 technology for control of nitrogen oxide
 (NOx) emissions, EPA sponsored the
 design,  construction,  and testing of a
 pilot-scale unit  (0.5  MW equivalent)
 which demonstrated  the operation of
 Hitachi Zosen's process on flue gas from
 a coal-fired boiler. This report gives
 details of the Hitachi Zosen process,
 designed to limit NOx emissions from
 coal-fired steam generators, and results
 of the demonstration program.
  This flue gas treatment (FGT) process
 uses selective catalytic reduction (SCR)
 of NOx  with ammonia which can
 achieve  over 90% reduction  in NOx
 emissions.
  Strict air pollution laws in Japan led to
 the  construction of several full-scale
 systems for the  removal of NOx from
 flue gas. Hitachi Zosen took the lead in
 this area with the construction of the
 first large  commercial unit in 1974.
 Hitachi Zosen now has nine commercial
 plants in operation.
  To further the goal of controlling
stationary source NOx emissions, EPA
sought to enhance the reliability and
effectiveness of  technology  to reduce
these emissions.  One aspect of EPA's
involvement includes  sponsoring pro-
grams designed to demonstrate this
technology. Because combustion mod-
ifications can achieve only limited

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reduction in NOx  emissions,  some
emphasis has been placed on developing
FGT processes.  In particular, SCR
technology appears to be a very promis-
ing method of reducing stationary
source NOx emissions by over 90%.
Consequently,  the EPA has acted to
demonstrate some of the more advanced
SCR systems.
  EPA initiated programs to demonstrate
two SCR processes on a 0.5 MW scale.
The processes  are:
    The Shell/UOP Simultaneous SOx/
     NOx Removal System.
    The Hitachi Zosen NOx Removal
    System.
The EPA-sponsored programs demon-
strated these processes on flue gas from
coal-fired boilers. The demonstration
programs were expected to  answer
many of  the questions which remain
concerning the application  of SCR
technology. In addition, these programs
should provide an improved basis for
estimating the costs of applying SCR
technology.

Process  Description
  One method of  removing NOx from
flue gas is using SCR. Ammonia is the
most  practical reductant  because it
reacts selectively and  quantitatively
with NOx to produce innocuous  nitro-
gen and water. Ammonia is available,
relatively inexpensive, safe to handle,
and easy to store.
  Ammonia will react with NOx without
a catalyst in a narrow temperature
range at  around 1000°C.  By  using a
suitable catalyst, the required tempera-
ture can be lowered to a more practical
range of 300-450°C.
  Carrier-based catalysts have been
developed and used by Hitachi Zosen in
several  plants in Japan. These are
pellets of alumina, silica, titania,  or
other materials into which the catalyst
is impregnated.
  With dust-containing  gases, carrier-
based catalysts are not practical because
the bed of catalyst will be plugged by the
particulate  matter  in  a  short  time.
However, parallel-flow  honeycomb
catalysts  have been developed and
applied to the removal of NOx from dusty
gases. These  catalysts permit lower
operating  costs because  of their low
pressure drops.
  The honeycomb catalysts developed
by Hitachi Zosen have been extensively
tested in several pilot plants and were
used  in this test  program. They  are
termed NOXNON   500  and NOXNON
600.
Overall Process Scheme
  The process consists of the injection
of a small amount of ammonia into the
flue gas and passage of the flue gas over
a catalyst. The ammonia reacts almost
entirely with the NOx in the flue gas to
form small quantities of nitrogen gas
and water  vapor, both of which are
normal constituents of the atmosphere
and are environmentally acceptable.
  Ammonia is injected into the flue gas
from a boiler between the economizer
and the air preheater (see Figure 1). At
this point the gas temperature is about
400°C which is suitable for the catalytic
reduction of NOx. This gas enters the
reactor, passes over  the catalyst, and
then reactions proceed. The flue gas
then  passes through  the  usual  air
heater, paniculate control, SOz control,
fan, and  stack. The ammonia for the
reaction is vaporized with steam and is
diluted with air (or steam) before
injection into the duct.  If the flue gas
temperature is too  low for  optimum
removal efficiencies, additional heat
can be added by auxiliary burners,  or
economizer bypass.

Chemistry
  The exact  relationships, between
ammonia and NOx are not completely
understood. However, certain reactions
are probably involved which may or may
not include oxygen. Virtually all of the
NOx in combustion gas is present as NO,
so the following equations are only for
NO reactions:
                                (1)
4NH3+6NO       = 5Nz+6HzO  (2)
  If NOz is also present, the following
reactions may also occur:
4NH3 + 2NOz+02   = 3N2+  6HzO{3)
8NH3 + 6NOz      = 7Nz + 12HzO(4)
2NH3+NO + NO2   = 2N2 +  3HzO(5)
  The reactions of ammonia with NOx
over the  catalyst occur below 300°C.
Without a catalyst the reaction will only
occur in a narrow temperature range of
                                         Temperature
                            r	/VOK	,  Recorder/
                               Recorder  \  Controller
                     Steam
                     or Air
                  Solenoid
                    Valve-
                    Vent"
                Flow Indicator/ Solenoid
                                                               Temperature
                                                                Recorder
                                               To S0» and Particulate
                                                 Control Systems
  Ammonia
   Boiler
Load Signal
Compressed
   Air
                    Flow Indicator/
                       Controller
Figure 1.     Typical commercial system flow diagram.

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 950-1000°C. Below this temperature
 the reaction rate is very low.

 Factors Affecting the Catalytic
 Reduction of NOx
   In any chemical reaction, there are
 factors which can influence the rate and
 extent of the reaction. These factors
 include  the reaction temperature,
 concentrations of reactant species, and
 other parameters specific to the reaction
 system. The following discussion briefly
 examines the major influences on the
 catalytic reduction of NOx by ammonia.
   The most  critical variables which
 affect the degree of NOx removal are the
 mole ratio of ammonia  to NOx, the flue
 gas flow rate, and the reactor tempera-
 ture.

Ammonia Emissions

  A small amount of  ammonia will
invariably pass through  the reactor and
exit with the flue gas due to incomplete
reactions between the  NOx and NH3.
Ammonia slippage (unreacted ammonia)
is of concern, and efforts  are normally
made to control slippageto levels of 10-
20 ppm. A high slippage of ammonia
can be considered a pollutant and, in
some cases in Japan, agreements with
local governments  have set allowable
levels at  around  10  ppm. Another
reason for the concern  with ammonia
slippage is that flue gas desulfurization
following  the denitrification system
could absorb any ammonia  in the flue
gas and ammonium salts can build up.
Bleeding of the ammonium  salts from
the system can cause water pollution
control problems in certain  cases. The
degree of slippage  is a  function of the
NHs/NOx mole ratio, the area velocity,
and  the  temperature  at which  the
reaction occurs. For commercial appli-
cation to coal-fired utility boilers,
ammonia slippage would be expected to
be less than 5 ppm at an  NOx removal
efficiency of 80%, and less than 10 ppm
at an NOx removal  efficiency of 90%.
Ammonium Sulfate/Bisulfate

  The presence of sulfur trioxide (SOs)
in the flue gas can lead to a reaction
with ammonia to form ammonium
sulfate and ammonium bisulfate. When
burning heavy fuel oil, approximately 2-
4% of the SOX in the flue gas are present
as SO3.  For coal combustion,  S03
accounts for approximately 1 % of the
total SOx. The reaction of ammonia with
this SO3 will  not  occur  above  about
300°C (572°F). At very low concentra-
tions, a temperature of around 200°C
(392°F) might be sufficient to avoid this
formation.
  To avoid such deposits it is necessary
that the temperature in the reactor be
maintained at a minimum of 320°C
(608°F) as long as ammonia is injected
into the reactor.
  The  formation of  bisulfate can  be
minimized to a large extent by maintain-
ing a low ammonia level in the flue gas
exiting the reactor. The presence of fly
ash also reduces the problem both by
scouring the deposits from surfaces and
by  providing surfaces on which  the
deposits will form instead of on metallic
surfaces.
Application of Process to
Boilers

  A  schematic flow diagram  of the
process as applied to a boiler is shown in
Figure 1. Flue gas leaving the economizer
at a temperature of about 390°C(734°F)
is first mixed with ammonia in quantities
needed to meet NOx removal require-
ments. The gas is then passed through
the fixed-bed catalyst reactor. No dust
removal is required prior to the catalyst
because of the non-clogging design of
the catalyst geometry. NOx  is reduced
by ammonia to innocuous nitrogen and
water. The denitrified gas then resumes
its passage through the normal boiler
train: air preheater, dust collection, etc.
  Ammonia required for the process is
first  vaporized with steam and then
diluted with either air or steam to aid in
the distribution of ammonia intothe flue
gas.
  The reactor is supplied with retract-
able  soot blowers  in which blasts  of
steam or hot air are occasionally applied
to the catalyst bed to remove deposits of
dust which may adhere to the surface of
the catalyst.

Catalyst Description
  A  particularly effective physical
design of the catalyst structure has
been developed by  Hitachi Zosen. This
structure  is  honeycomb shaped as
shown in Figure 2. Overall, the catalyst
has four characteristics:
  •  The structure is a  thin  plate
     honeycomb.
  •  Due  to  substantially reduced
     pressure drop across the catalyst
     layer,  operating power costs are
      much lower than with convention-
      al catalysts.
      A straight gas flow path prevents
      dust clogging.
      It is applicable for gases with high
      SO2 concentrations.
 Figure 2.    Configuration of NOXNON
             500 or 600 series catalyst.
  As a result, in treating high-tempera-
ture gases with high SOx and  dust
concentrations (such as coal-fired boi ler
flue gas), the NOx removal reactor can
be installed immediately downstream of
the economizer.  In addition, dust
elimination or other pretreatment is
unnecessary and, with the low pressure
drop, operating costs are low.
  The honeycomb catalysts are referred
to by Hitachi Zosen as NOXNON 500 or
NOXNON  600. These catalysts are
manufactured as plates and are fabri-
cated so as to form parallel flow gas
passages  which  provide  excellent
contact with the flue gas with minimum
impingement of fly ash on the catalyst
surface.
  The catalyst plates are  arranged in a
steel frame box supported by retainers.
A standard module is 1  meter long, 1
meter wide, and 0.5 meters deep. The
catalyst is activated after the corrugated
catalyst assembly is made.  In the
NOXNON 500 catalyst, thin stainless
steel  plates  are  used.  The  newer
NOXNON  600 catalyst,  instead  of
plates, uses a stainless steel wire mesh
as a base  metal  to give mechanical
strength upon which catalytic compo-
nents are cemented. The NOXNON 600
is considerably  lighter in weight and
contains more  active material for a
given volume of catalyst.

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  The active components of the catalyst
consist of vanadium and  titanium
compounds.  Other components are
added to increase resistance to fly ash
abrasion.
  The catalyst has an expected life of
about 2 years.  Regeneration of the
catalyst is not needed during the
planned catalyst life. At the end of the
useful life of the catalyst, it would be
removed from the reactor vessel and
scrapped. The catalyst does not contain
any  hazardous materials and can be
disposed of by recovering the metal in
the catalyst or by disposing of the spent
catalyst as industrial waste. No special
precautions are required in the disposal
process.

Reactor Design
  Reactor vessels housing the catalyst
are carbon steel and  are divided into
chambers each having its own fly ash
hopper (see Figure 3). Flue  gas flows
downward in the  reactor.  Flue gas
usually enters at the top of the reactorat
one  side,  passes  through the gas
distribution grid  and catalyst bed, and
exits the opposite side of the reactor at
the bottom. Fly ash that drops out of the
flue gas stream is collected in the
bottom fly ash hoppers and is disposed
of periodically.


Demonstration Program
  A potential market for the denitrifica-
tion of power plant flue gases may be at
coal-fired stations.  Limited test  work
has been done by Hitachi Zosen on flue
gas from coal combustion. The  EPA-
sponsored  demonstration at Georgia
Power Co.'s  Plant Mitchell was  an
excellent site for testing the Hitachi
Zosen process. The power plant burns
typically medium  sulfur coal  with
relatively  high  ash levels. Adverse
effects, if any, on the catalyst by this flue
gas could be readily evaluated.
  The demonstration plant was  highly
instrumented and provided much useful
data to supplement data collection from
previous work in Japan. Several param-
eters were evaluated, and their effects
on removal efficiencies and  ammonia
utilization were checked. The data were
collected and evaluated to  establish
valid characterizations of the process.
Long-term tests provided information on
the aging tendencies of the catalyst
when applied to flue gas from American
coal  burning  boilers. Additionally, the
data collected during these tests were
useful in establishing operating and
            Ammonia Feed
             Connections
                  Gas Distribution
                       Grids
             Catalyst

                    Soot Blower
    Treated Flue Gas to
     Boiler Preheater
Figure 3.    Typical reactor arrangement.
                                           Hoppers
capital cost requirements for commercial
installations.
  Hitachi Zosen, with  Chemico Air
Pollution  Control Corp. (CAPCC), a
Division of  Envirotech Corp.,  as their
major subcontractor,  provided the test
plant and  operated the unit. This
included detailed engineering, procure-
ment, fabrication, transportation, erec-
tion, test operation, and continuous
demonstration operation of the pilot
plant. The work was in four phases:
  Phase I (engineering) started with the
basic design  package which was de-
signed by Hitachi Zosen in Japan. Based
on these designs, CAPCC prepared a de-
tailed design.
  Phase II included start-up, debugging,
and parametric tests.
  Following the successful completion
of the system optimization test. Phase
III, the pilot plant was to be operated
continuously  (24 hours/day, 7 days/
week) for at least 3 months as Phase IV.
The period of continuous operation was
to include  no less than 75  days of
cumulative  operation in compliance
with contract objectives and  guaran-
tees.
  Additional tests were conducted as an
addition to  the original scope of work.
Phase V was  run  to  examine the
response of the SCR system's perform-
ance to transient operating conditions.
Schedule

  The period of performance for comple-
tion of the work related to the pilot plant
was originally 18 months. The award of
the contract was May 1978. The design
and specification period, Phase I, took
approximately 3 months.  Phase II re-
quired  approximately 9  months for
procurement, fabrication, transportation,
and erection. These schedules were as
originally expected. However, since start-
up  and debugging required about 2
months, the first tests were not started
until August 1,1979. This first charge of
catalyst  showed less than optimum
results after some 4 months of operation,
and it was decided  to replace  it  irr
December 1979. After some 4 additional
months of operation, the NOXNON 500
catalyst again began to provide less than
expected results, and a decision was
made to install a third charge of catalyst.
  The third charge was the new NOXNON
600.  This  was installed on April 18,
1980, and was used for some 9 months
until  the plant was shut  down on
February 2, 1981.


Description of the Test Plant
  The following description of the pilot
unit includes summaries of major items
of equipment (see Figure 4):
                                  4

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                    Flue
                 Gas Heater
Ammonia Supply
      Tank
              NH3
                                1.43 Ib/hr NH3
                                  fat 10 MR)
          Reactor

           J \  Soot Blower
         SOi
               /VO./SO, Generator
 Figure 4.    Process flow diagram of pilot 'plant.
                       Soot Blower
                        Gas Heater
               Fly Ash to
                                                     Vacuum Line
  Flue gas to be used as input to the
pilot plant was drawn from the boiler
duct downstream of the economizer and
introduced to the reactor through a 14-
in. diameter* pipeline.
  An electric heater was provided in the
piping between  the flues and the
reactor. This flue gas heater was used to
control flue gas temperature to the
reactor.
  Gaseous ammonia was injected to
the gas stream  after the heater and
before the reactor. The gas then flowed
down through the reactor  in contact
with the catalyst. The NOx  in the gas
reacted with the ammonia to form
small  quantities of  gaseous nitrogen
and water, which remained  in the gas
stream.
  Dust settling in the reactor was kept
within acceptable bounds, using a soot
blowing apparatus with either steam or
air.
  A blower, downstream of the reactor,
overcame  the flue gas pressure  drop
through the pilot plant. A cyclone dust
separator, ahead of the boiler, prevented
erosion of the blower by dust.
  Since it  was  planned to test the
performance of NOx, SOz, and SOs, and
since only fixed concentrations of these
('(Readers more accustomed to metric units are
  asked to use the conversion factors at the end of
  this summary.
substances were available from the
Albany, GA, plant boiler operation, SOg
was purchased for addition  to the flue
gas, and a NO,, SO2, and SO3generating
unit was provided to manufacture these
materials for addition to the flue gas.
This permitted testing at NOx, S02, and
80s levels  higher than those available
from the boiler.
  The operating conditions controlled in
the pilot unit are:
   • Flue gas flow rate.
   • Flue gas temperature.
   • The amount of charged ammonia.
   • Soot blowing gas pressure and
     temperature.

Host Site
  The  pilot plant was at  Unit  3  of
Georgia Power  Co.'s Plant Mitchell,
Albany, GA. This unit has a pulverized-
coal-fired  Combustion  Engineering
boiler,  initially operated on April 18,
1964, with a 125  MWnameplate rating.
The boiler has a rated steam  capacity of
1,075,000 Ib/hr of steam to the turbine
at 1800 psig. The unit is tangentially
fired with CE standard tilting bu rners for
steam  temperature control. The  pilot
plant was located outside Unit 3.

Data Collection
  The pilot  plant  operation was closely
monitored by an array of instruments
and analyzers. Continuous analyzers of
the latest design measured the NOx
levels  both  entering and leaving the
reactor.
  Much of the data  at the pilot  plant
were collected in a  data  logger which
frequently scanned the instruments and
stored  the data. Visual and paper tape
displays were  provided.

Relating the Results to a Full-
Scale Operation
  The  test unit included a section of
catalyst which had the same depth as
that to be used in a full-scale plant. The
results could therefore be  directly
extrapolated to a large plant assuming
that the  velocity,  mole ratio,  and
temperature remained the same and the
gas distribution  through the catalyst
bed was properly designed.
  Ammonia consumption could also be
determined from the test results because
it  is calculated as  a mole  ratio of
ammonia to NOX in the flue gas.


NOXNON 600 Tests

Introduction
  Primarily because of clogging of the
catalyst channels by fly ash  due to
narrow clearances,  the initial  and
second charges of  catalyst  did not
perform as expected. The installation
and testing  of NOXNON  600 catalyst
having wider channels was proposed by
Hitachi Zosen  and accepted by  EPA.
  NOXNON 600 is produced from thin
stainless steel wire  mesh (as a  base
metal to give  mechanical strength) to
which  catalytic components are ce-
mented. This technique  has  been
proven in applications on oil- and coal-
fired combustion flue gas in Japan.

Catalyst Performance
  Starting from  April  22,  1980, the
demonstration operation with NOXNON
600 ran for more than  9  months until
February 2,  1981. The operation with
combustion flue gas from the Unit 3
Boiler  of  Georgia  Power Co.'s  Plant
Mitchell was for 5620 hours.  The
program was terminated due to sched-
uled maintenance of the power  plant
requiring moving of the pilot plant.

  The  pilot  plant program required
achieving  NOx removal efficiency of
more than 90% continuously for more
than 3  months. Afterwards, the project
scope was extended and transient tests
were  included in  the scope  of the

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contract along with an extension of the
operating period.
  Catalyst life tests were run to confirm
the expected catalyst life. From April 22,
1980,  the pilot plant was operated
maintaining NOx removal efficiency of
more than 90% until the end of October.
After October,  a nominal 80%  NOx
removal  was  accepted  to decrease
ammonia slip as far as possible.
  Following the catalyst life test, further
testing was carried out to determine the
effects of transient conditions  on the
catalyst and to  provide  an extended
operating  time  so that at least 5000
hours of operation could be obtained to
evaluate the long-term effectiveness of
the NOXNON 600.
  At various times, tests were run  to
determine catalyst efficiency.
  During the operating time with flue
gas,  tests were run  including  catalyst
life tests, catalyst performance tests,
and transient tests. Controllability and
reliability of the entire system were also
evaluated at the same time.
  Operating conditions were varied for
the performance  and transient tests.
Therefore, when the activity of the
catalyst was to be evaluated, operating
conditions were set at certain consistent
levels each time. These conditions were
a flue gas flow rate of 1000 -1200 scfm,
a reactor temperature of 700 - 720°F,
and a NH3/NOx mole ratio of 1.0. Under
these conditions, the NOx removal ef-
ficiency was measured over a period of
several hours to determine the condi-
tion of the catalyst:
                         %Removal
At the beginning
of the operation              90 - 94
At the end of 8/80(2500 hours) 90 - 94
11780          (4000 hours)  90 - 92
Before transient
tests  12/80     (4420 hours)  90 - 91.5
During transient
tests 1/5/81    (5OOO hours) 90 - 91
After regeneration
1/27/81        (5500 hours) 91-94.5


Operating Variables

Mole Ratio
  During the test operation,  the pilot
plant was operated at a selected mole
ratio. The control system  was designed
to automatically provide this mole ratio
by using the flue gas flow rate signal
and the inlet NOx concentration analysis
to determine the quantity of  NOx in
the  inlet stream. From the inlet NOx
quantity  and the selected  mole ratio.
the required ammonia was automatically
calculated. This signal was then relayed
to the ammonia control system which
set the ammonia control valve setting to
provide the required ammonia flow.
  Figure 5 is a mole ratio curve which
shows that  80%  removal  requires a
mole ratio of  about 0.85,  while 90%
removal requires a mole ratio of  1.0.

Flue Gas Flow  Rate

  The NOXNON 600 catalyst for the
pilot plant was designed to operate at
1057 scfm, equivalent to an area
velocity (A.V.) of  9.6  Nm3/m2-hr.
However, operating at a much  higher
flow rate of 1650  scfm (an A.V. of 15)
provided the desired 90% NOx removal
efficiency. Therefore, it was anticipated
that between the designed  flow rate of
1057  scfm and the normal operating
flow rate of 1500 scfm, the NOx would
be unchanged.  As  seen in Figure  6, the
flow rate had little or no effect on NOx
removal.
Influence of SOx Concentration
on NOx Removal Efficiency
  Concentrations of SOx  measured in
the pilot plant deviated widely between
approximately 500 ppm and 1,500 ppm
depending on the variations of sulfur in
the coal.
  Through the whole operating period,
NOx removal efficiency was not affected
by SOx concentrations in the flue gas in
this relatively wide range.

Operating Temperature
  In the pilot plant, the operating
temperature was varied between 640°F
(338°C) and  780°F (415°C) without
affecting NOx removal efficiency. Opti-
mum operating temperatures from
fundamental experiments in the labora-
tory are between 572°F  (300°C) and
750°F (400°C).

NOx Concentration
  On August 24,1980, the NOxgenera-
tor was operated to increase the
  100
   80

I"
   20
                                                                     120
                                                                         .1
                                                                      40
             0.2     0.4      0.6      0.8     1.0
                            HN3/NOi Mole Ratio
               1.2
1.4
!                                                      01100 scfm 700±10°F
                                                      * 1300 scfm 700±10°F
                                                      01500 scfm 710± 5°f
Figure 5.    Effect of NHs/NO* ratio on /VO« removal efficiency and NH3 slippage.

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concentration of NOx at the inlet of the
reactor,  and the  influence  of  NOx
concentration was investigated.
  Between 400 ppm and 900 ppm  of
inlet NOx concentrations, the concen-
tration of NOx did not influence  NOx
removal efficiency. This data is consis-
tent with fundamental  data.

Ammonia Slippage
  Since a continuous ammonia analyzer
was not available  during the operation
of the pilot plant,  ammonia  had to  be
measured by wet analysis.
  Figure  5 shows ammonia slippage
when mole ratio was varied at operating
times of 3200 hours  to 4500 hours.
General conclusions from these tests
include:'
   • Flue gas flow rate had little effect
     on ammonia  slippage.
   • Ammonia slippage seemed  to
     increase slightly  with  increased
     operating time.
   • Ammonia slippage was apparent
     even at  low  mole ratios; e.g.,  at
     0.6.
  The reason for this  higher than
expected slippage may have been
clogging  by  fly  ash and  fibers  of
asbestos yarn used to  seal a clearance
between the catalyst box and  reactor.
These fibers, along with fly ash between
                                       the first and  second catalyst layers,
                                       probably reduced the effective catalyst
                                       surface  and adversely affected  the
                                       apparent catalyst activity resulting in
                                       relatively high  ammonia slippage. Even
                                       a slight reactivity loss, while producing
                                       little loss in NOx removal efficiency, can
                                       significantly increase ammonia emis-
                                       sions.

                                       Oxidation  of SO2 to SO3
                                         On July  23-25, 1980, operating
                                       conditions were maintained constant so
                                       that  S03  measurements could  be
                                       obtained at  the inlet and outlet of the
                                       reactor.
                                         The results indicated an  average
                                       oxidation rate of 1.8%.
                                         Prior  experimental results indicated
                                       that,  at these conditions, the ratio
                                       should have been somewhat lower: 1.0
                                       - 1.5%.

                                       Transient Tests
                                         After the  NOx removal efficiency of
                                       more than 90%  was demonstrated in
                                       the continuous  run  of 3 months as
                                       required in the contract, a decision was
                                       made to extend  the scope of  the
                                       contract. This was done to supplement
                                       the originally planned operation of the
                                       pilot  plant  to further establish  the
                                       suitability  and  reliability of  Hitachi
   100
    90
u
.§
.S
2
o
I
i
    80\-
    70
                                     Reaction Temp.:  Approx. 7OO°F
                                     NHs/NO* Ratio: Approx. 1.0
                                     Symbol Operating Period
                                      fo   200
                                      ,• 2/50
1250hr
3750 hr
            WOO    1100   1200   1300    1400   1500    1600    1700

                               Flue Gas Flow Rate, scfm



Figure 6.    Effect of flue gas flow rate on /VO« removal efficiency.
Zosen's catalyst for commercial opera-
tions on coal-fired combustion flue gas.
Five transient tests were performed.

Emergency Shut-off of
Ammonia Feed
  The EPA pilot plant was provided with
a trip system for ammonia supply. The
purpose of the trip system was to shut
off the ammonia feed when tempera-
ture in the reactor decreased to 600°F
and allow it to introduce ammonia into
the system when temperature in the
reactor increased  and returned  to
600°F. The purpose of this test was to
confirm the reliability of the trip system.
  The results of this test proved that:
• Automatic shut-off and supply of am-
  monia  operated smoothly.
• NOx removal efficiency and pressure
  drop at a temperature of 700°F was
  constant and unchanged through the
  three repeated tests.

Cold  Start-up
  A commercial boiler normally starts
operating after a long shutdown with
the reactor and  ductwork filled with
ambient  air  When  operation com-
mences, flue gas is introduced into the
system as the temperature rises and the
flue gas can be relatively cool for a time
when in contact with the catalyst. There
is a risk of formation and deposition of
sulfuric acid mist, ammonium sulfate,
and ammonium bisulfate. Previous
experience proved that sulfuric acid
mist  does not deteriorate the catalyst,
and ammonium sulfate and ammonium
bisulfate  can be  removed when the
temperature rises. The purpose of this
test was to prove that cold start-up with
flue gas does not affect the NOx removal
reaction.
  On  December 27, 1980, the  blower
was started and flue gas was introduced
into the system directly. The system was
heated up with flue gas and put into
operation.
  Twelve hours after commencing the
start-up,  operating conditions  became
stable  at  the same conditions before
cold  start-up  The results proved that
cold start-up does not influence catalytic
performance.

Boiler Shutdown and Start-up
  From time to time a power plant boiler
shuts down and starts up, and an NOx
removal  system must follow such
transitions.
  The  purpose of this test  was  to
confirm the controllability of the NOX
removal system during the  shutdown

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and start-upof the boiler. When the host
boiler was shut down for maintenance,
this test was executed with the NOx
removal  system shutting down and
starting up along with the boiler with no
purging  of the  reactor.  The results
proved that the system could withstand
the transient shutdown and start-up of
the boiler.

Sudden Load Change
  A power plant boiler may occasionally
change load suddenly, complying with
variations of power consumption. The
NOx removal" system should  follow
these sudden boiler load changes. Two
levels  of operating conditions were
adopted as representative load levels:
•  High load: 1,300 scfm, 700°F, 0.8
   mole ratio.
•  Low  load: 900  scfm, 610°F,  0.8
   mole ratio.
  The  above conditions were altered
every 2  hours  and continued  for 24
hours. No serious problem seemed to be
caused by these sudden load changes.

Sootblower Requirements
  From the   beginning  of pilot plant
operation with the third charged catalyst,
NOXNON 600, the sootblower was
operated three times a day, one cycle at
a time, to prevent clogging by fly ash.
This frequency seemed to be the mini-
mum  to  prevent clogging; however,
there  was no experience in operating
the pilot plant without the sootblower.
Thus, a trial was made to operate with-
out the sootblower.
  At a flow rate of  1,100 scfm, 700°F,
and 0.8 mole ratio, sootblower operation
was halted and the progress of pressure
drop increase was  observed. Pressure
drop  appeared  unstable  (increasing
gradually from 1.20 to 1.25 in.  H20 to
1.35 to 1.40 in. H2O in approximately 28
hours) and seemed to  continue to
increase. The  sootblower was  then
restarted.  This test  indicated that
operation of the sootblower was neces-
sary.

Changes in Pressure Drop in
Relation to A/Ox Removal
Efficiency
  In the treatment of coal-fired combus-
tion flue gas, it is realized that adhesion
and clogging caused by fly ash, along
with the formation and deposition of
ammonium sulfate  and bisulfate, cause
problems. In NOx  removal systems,
these problems are first noticed as an
increase in  pressure drop. Therefore,
changes in pressure drop were carefully
studied during the operation of the EPA
pilot plant.
  Since operating conditions  varied
from time totime in accordance with the
needs of the  pilot plant operation and
the scope of  the contract,  changes of
pressure drop were evaluated by a ratio
of measured value to a calculated value.
  Several experiments were carried
out.  The tendency for pressure  drop
changes is summarized below.
• When the pilot plant was shut down,
  for some reason the pressure drop
  generally  increased  after  the  next
  startup. The increased pressure drop
  usually continued at this high  level
  although the sootblower was oper-
  ated three times a day. However, the
  previous pressure drop was restored
  after a few days  of  continuous
  operation.
• When the  flue  gas flow  rate was
  changed, the pressure drop increased
  at times. For example, in November
   1980 after some 20 days  of steady
  operation the flow rate was changed
  from 1300 to 1500 scfm and after 2
  days  at  this higher flow rate the
  pressure drop  suddenly increased
  and did not return to its original level
  for several  days.
• Whenever  Georgia  Power's  Unit  3
   boiler operated the economizer
   sootblower repeatedly, the pressure
  drop across the catalyst  increased.
• On December 18, 1980, the water
  tubes of the boiler were washed with
  pressurized water to remove  slag on
  the tube surface while the boiler was
   in operation. This abnormal mainte-
   nance work caused a serious increase
   in pressure drop.
• Operation of the sootblower seems to
   be necessary for coal-fired combus-
  tion flue gas. The  pilot plant was
  operated for 28 hours  without the
   sootblower, and the pressure drop
   increased  sharply.  After  the soot-
   blower was returned to  operation, it
   took 3 days to  restore the pressure
  drop.

Regeneration of Catalyst
  When the catalyst was washed with
warm water,  NOx removal efficiency
was restored to its initial efficiency. The
pressure drop also seems to have been
partially restored. However, the catalyst
was partially clogged with  asbestos
fibers, which  is not typical. The effec-
tiveness of water washing for pressure
drop restoration, therefore, is u ncerta i n.
Also, the waste wash solution contains
dissolved metals from the fly ash which
would require water treatment before
disposal.

Abrasion of Catalyst
  Among  the  four blocks  of  catalyst,
only some of the flat plates in the top
block showed  a  loss  of  catalyst  by
abrasion. This was probably due to the
vibration of the loose plates caused by
the impact of the flue gas  flow. There
was no abrasion in the other blocks. A
commercial system would incorporate a
tighter catalyst structure to avoid such
vibration.

Clogging
  Anticipated clogging of the catalyst by
fly ash was prevented by operating the
sootblower three times a day. Reducing
this frequency of operation may be
possible  but  it was not tested. Apart
from the clogging anticipated by fly ash,
asbestos  fibers unfortunately  led to
plugging of about 30-35% of the catalyst
passages between the top  catalyst
blocks and the second  catalyst blocks.
This was caused by asbestos rope used
to seal passages between  the catalyst
box and the reactor shell. This asbestos
would not be used  in  a  commercial
plant.

Conclusions
  The contract  objectives were ex-
ceeded. NOx removal efficiency of more
than 90% was demonstrated during an
operating period of about 5000 hours at
the  designed  capacity of 0.5 MW
equivalent.  Following this period,
transient tests were run. These demon-
strated that the performance was  not
adversely affected by such conditions as
sudden boiler load changes, cold start-
ups,  low boiler  loads, or  by  boiler
shutdowns  and start-ups. The pilot
plant operation  was terminated after
5620  hours  of  cumulative  operating
time only because the host  boiler had to
undergo major modifications necessita-
ting that the pilot plant be  moved.
  During  operation of  the pilot plant,
catalysts had to be replaced twice. The
first and second charges of catalyst had
relatively  narrow clearances  between
the catalyst plates and were clogged by
fly  ash from  the flue gas resulting in
increased pressure drops  through  the
catalyst beds. There was also a  slight
decrease  in apparent catalyst activity,
although true catalyst activity did  not
decrease. These catalysts, which were
NOXNON 500, had been tested in pilot
plants in Japan for application to coal-
fired  combustion flue gases from

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boilers prior to application to the EPA
pilot plant. However, clogging caused by
fly  ash was  not  experienced even
though no sootblower was installed or
operated in those pilot plants.
  There  were obviously significant
differences in the character and compo-
sition of the  fly ash in the U.S. as
compared to that in Japan.
  Nevertheless, the tests with NOXNON
600 were  highly successful.  This
catalyst has somewhat wider clearances
between the catalyst plates, helping to
avoid fly ash clogging problems.
  Fly ash contained in flue gas varies in
its characteristics and behavior relative
to its clogging tendency in catalyst beds.
This depends on the source and compo-
sition of the coal. At present, qualitative
measurements to estimate the tenden-
cies to agglomeration and cohesion of
fly ash are available  through chemical
analysis and thermal processing tests.
However, more adequate and accurate
methods to estimate  the behavior of fly
ash in catalyst beds will be required. It is
expected that this method when further
amplified will be  useful in selecting
adequate linear velocity to prevent
clogging and abrasion caused by fly ash,
and  to  determine the  necessity  and
operating conditions  of the sootblower.
Improvement of  catalyst configuration
to prevent  clogging by fly ash is  also
expected.
  Testing for catalyst regeneration by
washing  was examined just before the
pilot plant was dismantled. The results
were very encouraging. The regenerated
catalyst exhibited properties of a virgin
catalyst.  However, due  to the limited
time  available, potential problems
related to  the catalyst  regeneration
were  not clarified.  For  example, the
method of drying the catalyst and the
reactor after regeneration without
encountering corrosion or fly  ash
clinging,  and  the treatment of waste
washing solution should be investigated
before commercial  application. This
area should be studied further since the
cost of this technology  could be sub-
stantially reduced  if the catalyst  life
could be extended by in situ regeneration
techniques.
  Based  on tests with  NOXNON  600
both at  the  EPA  pilot  plant and in
Japanese pilot plants, 90% NOX removal
could be expected at a NH3/NOx  mole
ratio of 0.92 - 1.0. Although ammonia
slippage from  the  EPA pilot plant
measured about 40  ppm under these
conditions, ammonia  slippage would be
expected to be less than 10 ppm based
on Japanese tests. The differential was
probably due to the asbestos clogging in
the  EPA  pilot plant.  For 80% NOx
removal the required mole ratio would
be 0.82 - 0.85 with ammonia slippage of
5 ppm or less, again based on tests in
Japan.
  The pressure drop with NOXNON 600
catalyst in the pilot plant and expected
commercially is only 1.0-1.4 in. HzO.
Such low pressure drops required very
little power consumption  resulting in
low operating costs.
  The controllability  of the pilot plant
was satisfactory. However, the control
system  for commercial plants  would
differ slightly from the pilot plant control
system due mainly to the problems in
measuring flue gas flow. The reliability
of the system was very good as verified
by the high onstream factor achieved. A
desirable addition to the control system
would be  a  continuous  analyzer to
monitor slippage of ammonia.
  The  NOx removal  efficiency of this
SCR system in commercial applications
would be expected to be the  same as
that experienced in the EPA pilot plant if
the  size  and configuration  of the
catalyst, superficial linear velocity of the
flue  gas  across  the  catalyst, and the
temperature of flue gas were the same.
Therefore, the data is directly applicable
for scaling of commercial systems.
  The pilot plant project was the first
demonstration and evaluation  of  NOx
SCR technology on a coal-fired source
in the U.S. The project results  indicate
that the process may be usable as a NOx
control option; however, some technical
concerns remain before the technology
can be considered commercially avail-
able and  demonstrated for coal-fired
sources in the U.S.

Metric  Conversion
  Readers more  familiar  with metric
units are asked to use the following
factors to convert certain  non-metric
units used in this summary.
 Non-metric Multiplied by Yields metric
     °F     5/9(°F - 32)      °C
     ft3         28.3         1
     in.         2.54         cm
     in.2         6.45        cm2
     Ib         0.45         kg
  Shingo Tanaka is with Hitachi Shipbuilding & Engineering Co.. Ltd., Palaceside
    Building, 1-1, Hitotsubashi, 1-Chome, Chiyoda-Ku, Tokyo, Japan and Richard
    Wiener is with Chemico Air Pollution Control Corporation, New York, NY
    10001.
  J. David Mobley is the EPA Project Officer (see below).
  The complete report, entitled "Hitachi Zosen NO, Flue Gas Treatment Process:
    Volume 1. Pilot Plant Evaluation," (Order No. PB 83-113 829; Cost: $20.50,
    subject to change) will be available only from:
          National Technical Information Service
          5285 Port Royal Road
          Springfield, VA 22161
           Telephone: 703-487-4650
  The EPA Project Officer can be contacted at:
          Industrial Environmental Research Laboratory
          U.S. Environmental Protection Agency
          Research Triangle Park. NC 27711

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