United States
                    Environmental Protection
                    Agency
Industrial Environmental Research
Laboratory
Research Triangle Park NC 27711
                    Research and Development
EPA-600/S7-82-065a Mar. 1983
<&Efir\          Project  Summary
                    The  Adipic Acid  Enhanced  Flue
                    Gas  Desulfurization   Process  for
                    Industrial  Boilers:
                    Volume  1.  Field Test Results

                    P. A. Clarke, R. W. Gerstle, D. S. Henzel, K. W.  Mason, and S.  R. Sabatini
                      This study evaluated the  effect of
                    adding adipic acid on the SCfe removal of
                    a wet limestone flue gas desulfurization
                    (FGD) system on a coal-fired  industrial
                    boiler at Rickenbacker Air  National
                    Guard Base near Columbus, OH. Emis-
                    sion data were collected in accordance
                    with the regulations for SOa compliance
                    data specified in  the Federal  Register.
                    Test results show that adding adipic
                    acid to the limestone slurry significant-
                    ly improved the SOj removal efficiency
                    of the FGD system. Limited baseline
                    data on operations with limestone only
                    indicated a performance level of 55
                    percent  SO2 removal. Adding about
                    2200 ppm of adipic acid to the lime-
                    stone scrubbing systems, the unit's level
                    of performance increased to an average
                    of 94.3 percent SO2 removal which was
                    maintained within a standard deviation
                    of 2.2 percent over a 30-day test period
                    during which boiler load was  70 - 130
                    million Btu/hr and gas throughput
                    varied 300 percent.
                     This Project Summary was  devel-
                    oped by EPA's Industrial Environmen-
                    tal Research Laboratory. Research Tri-
                    angle Park. NC, to announce key find-
                    ings of the research project that is fully
                    documented in a separate report of the
                    same title (see Project Report ordering
                    information at back).

                    Introduction
                     The report describes how the addition
                    of adipic acid to a wet limestone scrubber
                    system affects  sulfur dioxide  (S02) re-
                    moval efficiency.  The site selected for
                    the test, Rickenbacker Air National Guard
 Base (RANGB) near Columbus, OH, has
 six spreader-stoker boilers with a total
 capacity of 222 GJ/h (210 x 106 Btu/h).
 The boilers produce hot water, primarily
 for space heating.  S02 emissions are
 controlled by a scrubber system manu-
 factured  by   Research-Cottrell  under
 license from A. B. Bahco of Sweden. The
 FGD system, shown in Figure 1, consists
 of a mechanical collector, Swedish Bahco
 scrubber tower, limestone storage and
 handling  system,  clarifier  (thickener),
 booster fan, sludge disposal pond, and
 associated ductwork, pumps, and con-
 trols.  Table 1 gives key design parame-
 ters for the scrubbing system. During the
 test a mechanical dry feeder introduced
 the adipic acid into the scrubber system
 at the same location where fresh lime-
 stone is added.
   Untreated flue gas from the individual
 boilers enters a common header equipped
 with a bypass stack and is fed through a
 mechanical collector for primary removal
 of particulates. The design removal effi-
 ciency of the mechanical collector is 70
 percent. A fan then introduces the par-
 tially cleaned flue gas into the scrubbing
 tower for SC>2 removal.

  The Bahco scrubber is a tower con-
sisting of two inverted venturi scrubbing
stages.  Untreated gas entering the first
stage is diverted down to impinge on the
liquid slurry surface of the mill.  The gas
then rises through the first stage venturi,
where it intimately mixes with the slurry
droplets now entrained in it The partially
scrubbed gas is then diverted down onto
the liquid slurry surface  in the second-

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Table 1.    Design Process Information for Rickenbacker Air National Guard Base
	Scrubbing System	
Total rating
Number of boilers
Boiler capacity
Number of separate FGD units
Control system vendor
Type of FGD system
Start-up date
SO2 removal efficiencies

Paniculate removal efficiency
Water makeup
Sludge or by-product disposal
2600 Nm3/s f55,000 scfm)
6
222 GJ/h (210 x 1& Btu/h)
1
Research- Cottrell/Bahco
Retrofit
March 1976
90%+ design  with lime operation; lower
with limestone operation
98% design
Open loop
Unstabi/ized CaS03/SO4 sludge to lined
pond	
 stage pan, and the process is repeated.
 The treated gas is then directed up into a
 cyclonic mist eliminator, where entrained
 slurry droplets are removed  before the
 gas exits through  a  stub stack to the
 atmosphere.
   A certified extractive continuous emis-
 sion monitor (CEM) system and an onsite
 computer measured and recorded con-
 centrations of SC>2 and 02 in the flue gas
 stream.  Equipment at RANGB includes a
 continuous SOa monitoring  system  on
 the scrubber, which was used during the
 test after some maintenance work and
 calibration. Research Triangle Institute,
 under contract to EPA, audited the moni-
 toring system on March 5 and 6, 1981,
 and found it to be operating  properly.
   Both the certification (based on Federal
 Register procedures) and internal audits
 (based on certified 862 and 02 gases)
 showed that the monitors were operating
 properly.  Some problems entailing un-
 scheduled maintenance were  encoun-
 tered during the initial 168-hour monitor
 conditioning period. Also, on  March 20 a
 small leak was discovered  in the SO2
 monitor  internal valving system.  Appar-
 ently, rich inlet gas had leaked through
 this valve into  the outlet gas  sample
 stream, causing a slightly higher outlet
 SC>2 concentration reading and  corres-
 pondingly lower calculated SO2 removal
 efficiency.  The extent of the leak was
 determined by introducing audit gases
 and making manual S02 tests of the flue
 gases; a correction factor was applied to
 the outlet readings from March 18 until
 the leak was repaired on April 3.

 Test Procedure
   The adipic acid  test period at  RANGB
 was from February 9  to April 10, 1981,
 during which time the equipment was set
 up and calibrated and data were collected
 The monitoring equipment began operat-
 ing on  February 13, but the first few
 weeks of the test were used for shake-
  down and calibration of the monitors. The
  data collected  included measured SC>2
  and 02 concentrations in the gas stream
  at the  scrubber  inlet and  outlet and
  chemical analyses of the scrubber slurry,
  limestone, and coal. Scrubber and boiler
  operating conditions were recorded sev-
  eral times daily.
    The adipic acid feeder was set up for
  continuous addition of the adipic acid to
  the slaker--the  same location  at which
  fresh limestone is added.  When large
  quantities were necessary to increase
  slurry concentrations, the adipic acid was
  manually  introduced  directly  into the
  thickener tank because the sudden addi-
  tion  of adipic acid in large quantities to
  the slaker caused foaming in the slurry.
  This did not occur in the thickener.
    Slurry was analyzed at the site,  but
  periodic samples  were also  checked at
  the Base laboratory for quality control.
  The adipic acid analytical procedure uti-
  lized silicic acid and provided the con-
  centration of all carboxylic acids, not just
  adipic.  As indicated by the  numbers in
  Figure 1, liquid samples were taken at
  (1)the  limestone slurry feed  into  the
  scrubber, (2) the second-stage level tank,
  (3) the mill recycle loop (known as the'
  mill pump sample), (4) the thickener inlet
  stream,  (5) the  thickener overflow, and
  (6) the thickener underflow stream.  Be-
  cause the limestone slurry feed sample
  was  used as a control  sample, it was
  taken twice a day. The mill pump sample
  was taken once a  day, and samples were
  taken from all six  locations once a week.
  Slurry solid samples,  taken  by filtering
  samples from the  liquid sample streams,
  included the limestone slurry feed (once a
  week), the thickener inlet (three times a
  week), and the thickener underflow(once
  a week, usually while sludge was being
  pumped to the  settling  pond).   Coal
  samples were  taken  once  a  day, and
  limestone samples were taken  once a
  week. The coal samples were combined
into weekly  composites  before  being
analyzed.
   For  highest  S02 removal  efficiency,
best limestone  utilization, and most effi-
cient use of adipic acid, optimum scrubber
operation was maintained by keeping the
pH of the limestone dissolver tank slurry
near 5.0.  This was done by manually
adjusting  the  limestone  feed rate  to
correspond with changes in  the  boiler
load.  Except during occasional upsets in
scrubber operations, the adipic acid feed
rate remained constant at a concentra-
tion of 2000 - 2500 ppm throughout the
test. On March 20 and 21  the limestone
feed rate and adipic acid concentrations
were increased  in an effort to achieve still
higher S02 removal efficiency.
   From March 4 to April 10 the test was
interrupted only twice because of scrub-
ber operation. On March 23 the electrical
power to the scrubber was interrupted,
and on March 30 the scrubber was shut
down  because  the thickener tank had
plugged (apparently as the  result of some
plastic  sheeting)  and  remained  down
until 8 a.m. on  April 1.  On April 10 the
addition of adipic acid was stopped, and
the continuous  monitoring program was
terminated.   Sufficient data  had  been
accumulated  by that time, and warmer
weather was  resulting in increasingly
reduced boiler  loads.

Quality Assurance  Plan for
Continuous Monitoring
  PEDCo performed a quality  assurance
check on the continuous emission moni-
toring system (CEMS) to ensure the reli-
ability  of the data  collected. The check
consisted of two distinct but equal func-
tions: (1) assessment of the  quality  of
the CEMS data  by  estimating precision
and accuracy, and (2)  the  control and
improvement of the quality of the CEMS
data by implementng  quality control
policies and  corrective actions.   The
second function was related to the first in
that determination  of data quality inade-
quacy  resulted  in  an  increase in the
quality control effort until the  data were
considered acceptable.
  The  field  operations included  stan-
dard daily procedures for ensuring that
the following activities were performed
adequately.


Calibration of the CEMS
  The CEMS was calibrated with gases of
known  S02 concentrations. Two  gases
and ambient  air were  run through the
analyzer for each  test  mode  (inlet and
outlet).  The results of each  were  re-

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                                                  Sfac* •
     Adipic
     Acid
     Feeder .
  Limestone — — J|
   Feeder     Tl—I
Limestone,
  Truck
          ~"b
                                         Makeup
                                         Water
                   t
                   t
                                                                       Outlet SO2 Probe
                                                                                          Thickener
                     .Limestone
                      Storage
                                 Overflow to
                                 Limestone
                                    Feed
                                    Tank
                                                                                            To Mill
                                                                                            Sump
                                                                                                 Seal
                                                                                                Water
                                                                                                   Sludge
                                                                                                   To Pond
                                                           • Bypass
                                                         Makeup Stack
                                                                 Flue Gas
                                                                From Heat
                                                                   Plant
        Unloading
         Station
                                                                          Mill Pump
                                                                      Recycle From
                                                                   Thickener Underflow
Figure 1.   Flow diagram of the scrubber system at ftickenbacker.
corded, and any necessary adjustments
were made.
  All activities  involved  in routine cali-
bration and adjustment of the CEMS were
recorded daily in a standard calibration
data log.

Calibration of Drift
Determination
  Daily initial calibration readings for all
CEMS  zero and span values were com-
pared with the final calibration readings
of the preceding day to determine if any
change had occurred in 24 hours. Seven
consecutive sets of these initial/final
readings were recorded for each parame-
ter to determine 24-hour drift

Preventive Maintenance for
CEMS
  The CEMS was regularly inspected for
problems that might lead to loss in opera-
bility or data quality.  Each day the four
separate systems  of  the  CEMS  were
checked independently:  the SO2 analy-
zer, the 02  analyzer, the instrument
recorders, and the sampling interface.

Program of Corrective Action for
Malfunctioning CEMS
  Any  CEMS  malfunctions discovered
during  preventive  maintenance  checks
prompted immediate corrective action. A
complete log of all CEMS malfunctions
and corrective actions was maintained.

Accuracy Assessment
  PEDCo performed relative  accuracy
tests on the  CEMS according to EPA
reference methods and system  audits
with EPA-tested audit gases based  on
Standard Reference Materials (SRM).
  Figures 2 and 3 show the locations of
the CEM probes and reference method
sampling ports for the inlet and outlet
Inlet and outlet sampling locations were
selected to represent the streams tested
and  to  achieve  equivalence between
manual  and CEMS samples.
  Performance Specification Test Regu-
lations require that a minimum of 9 and a
maximum of 12 sets of reference method
data be  taken at  a rate of no more than
one set per hour. Regulations also require
that  the analyzer  monitor  stack  gas
concentrations continuously during refer-
ence method testing.
  All  data  derived  using  the reference
method  and the continuous monitor are
given on a  dry basis; a moisture correc-
tion factor  is used  to give results on a
consistent basis.  SO? and oxygen tests
were run simultaneously.  The CEM anal-
ysis of moisture content was determined
by measuring the temperature of a sample
taken after the moisture trap in the samp-

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                                  Reference Method
                                    Sample Ports
Continuous Reference

;*.» A
lathnei
Probe Ports
i


Induced
Draft
Fan

I
76 cm £
V
. 	 IT
nl
JO in.) H
11
J

^r^^"Tr"
f
129.5 cm
(51 in.)
•
	 — J 	 — ^
u 	 722 cm 	 frL — 760 c/r?_.
1 (48 in.)
(63 in.)




Scrubber
Module


Figure 2.    Scrubber inlet sampling locations.
ling system.  Moisture content was then
calculated because the gas stream being
analyzed was saturated.
  Tables 2 and 3 give the relative accura-
cy data for the initial certification period.
 Relative accuracy, based on nine sets of
 reference method data, was  calculated
 according to  equations in  Section  7,
 Appendix B, Federal Register, Vol. 44,
 No. 197. These calculations showed that
 the relative accuracy at the inlet was 1.72
 percent (based on  S02 concentrations)
 and 7.30 percent (with S02 expressed on
 a  weight per heat  input basis).  The
 corresponding  values  at the scrubber
 outlet  were 18.67  and 16.43  percent,
 respectively.

 Performance Audits
   Performance audits were conducted to
 maintain quality control throughout the
 monitoring period.  Audit gases certified
 by the EPA  were  introduced  at the
scrubber inlet through a manifold pres-
surized to 3.39 kPa(1  in. Hg) to duplicate
sampling conditions.  Audit gases were
introduced at the scrubber outlet through
an open-end manifold at ambient atmos-
pheric  pressure.   No adjustments were
made to the analyzer flow rates.  Analyzer
response to audit concentrations  was
determined  by  the  computer  used for
storage and retrieval of the  emission
monitoring  data.  Results of these tests
showed  excellent agreement  between
the audit gas concentrations and analyzer
readings for SOa and  oxygen at both the
inlet and outlet

Results
  Table 4 summarizes the daily average
SOa  monitoring data for those 30  days
when 18 hours  or more of acceptable
readings were obtained and  high effi-
ciency was achieved.  These data show
that  94.3 percent was  the mean
removal efficiency, with a corresponding
standard deviation of 2.1. These data do
not include days when the limestone feed
rate was low  or when other known
operating problems occurred.  The emis-
sion values are based on an F factor of
2.63 x 10'7  m3/J (9780 dscf/106 Btu).
The average inlet SOa loading for the test
period was 2125  ng/J (4.94 lb/106 Btu)
of heat input to the  boiler; whereas, the
average SOa outlet value measured was
122 ng/J (0.28 lb/106  Btu).  Limited data
obtained on February 12  - 16,  before
adding  adipic  acid, showed  scrubber
removal efficiency of 45 - 65  percent.
  Analyses of the coal burned during the
initial monitor operating period and the
test period are shown  in Table 5.  These
data show that the coal sulfur content
during the continuous  monitoring period
was 2.22 - 3.55 percent by weight on a
dry basis. Based on these data, the calcu-
lated SOa emission  rate (assuming that
95 percent of the sulfur is  converted to
SO2) was 1299 - 2210 ng/J (3.02 - 5.14
lb/106 Btu).
  The average daily feed rates for lime-
stone and adipic  acid  for the  entire test
period are shown in Table 6.  This table
also gives the quantity of coal used per
day, which  indicates the  variation  in
boiler  load.  From March 4 to April  10,
1981, coal usage varied from 60.8 to 138
Mg/day (55 to 125  tons/day), reflecting
the effect of changes in daily temperature
on the boiler heat  output  demand.   Of
particular  interest is the ratio of  adipic
acid to limestone used  to  maintain the
high SOa removal efficiencies during the
test the ratio varied from 6 to 30 g/kg(12
to 60 Ib/ton)  and averaged 1 2 g/kg (24
Ib/ton).  Uniform limestone and  adipic
acid addition  was  difficult to maintain
because of the use of manual controls,
the  varying  boiler  load, and the inter-
mittent discharge of sludge to the holding
pond.

Conclusions

  The project resulted in the successful
completion of a certified continuous SOa
monitoring performance test which veri-
fied  that the addition  of adipic acid did
enhance the  SOa removal  capability of
the Rickenbacker FGD limestone control
unit without having any adverse effect on
operating  parameters.  Before the test,
this  limestone  scrubber was achieving
about  55  percent  SOa  removal.  The
adipic acid additive increased the unit's
SOa removal  efficiency to 90  - 97.4
percent (averaging 94.3 percent)  over a
30-day test period.

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  Reference
   Method
     Train
 166.4 cm (65.5 in.)
  Inside Diameter
                 Continuous
                   Monitor
                        Reference
                         Method
                         Sample
                           Port
                                                                       Continuous
                                                                      ^ Monitor
                                                                        Location
Figure 3.    Scrubber outlet sampling locations.
Table 2.
Inlet Reference Method and CEM Results
                                                   Reference method
                                                                                               Monitor3
Test Vmb (std) (JO-4
No. Time NrrP
RIC-1 O749-O819 O.O251
RIC-2 0926-0951 O.0257
RIC-3 1010-1035 0.0254
RIC-4 1110-1135 0.0257
RIC-5 1210-1235 O.0254
RIC-6 1310-1335 0.0274
RIC-7 1410-1435 O.0277
RIC-8 1510-1535 0.0265
RIC-9 1610-1635 O.0278
RIC-10 1710-1735 0.0286
a Three monitor readings taken
(dscf)
(0.888)
(0.908)
(0.897)
(0.908)
(0.896)
(0.967)
(0.979)
(0.937)
(0.982)
(1.01)
g/Nm3
2.03
2.15
2.11
1.94
1.76
2.02
1.92
1.83
1.83
1.86
during reference
Ib/dscf)
(1.27)
(1.34)
(1.32)
(1.21)
(1. 10}
(1.26)
(1.20)
(1. 14)
(1. 14)

method run.
SO2,
ppm
775
816
802
734
671
766
753
693
697
703
(ib soy
ng/J
1965. 1
1849.0
1849.0
1840.4
1831.8
1763.0
1737.2
1732.9
1732.9
1775.9
Monitor readings
106 Btit
(4.57)
(4.30)
(4.28)
(4.28)
(4.26)
(4. 10)
(4.04)
(4.03)
(4.03)
(4. 13)
were then
<) %O2
15.2
14.5
14.6
15.1
15.6
14.6
14.6
15.1
15.1
15.1
averaged
S02,
ppm
753
803
805
736
668
793
768
694
689
707
for final
(ib soy
ng/J
1930. 7
2132.8
2029.6
1887. 7
1711.4
1874.8
1874.8
1874.8
1797.4
1724.3
emission
10s Btu)
(4.49)
(4.96)
(4. 72)
(4.39)
(3.98)
(4.36)
(4.36)
(4.36)
(4. 18)
(4.01)
results.
%02
14.9
15.1
14.8
14.9
14.9
14.4
14.6
15.2
15.0
14.6

b Vm = metered volume (dry basis).

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Table 3.
Outlet Reference Method and OEM Results
                                               Reference method8
                                                                                          Monitor
Test
No.
ROC-1
ROC-2
ROC-3
ROC-4
ROC-5
ROC-6
ROC- 7
ROC-8
ROC-9
ROC- 10
ROC- 11
ROC-1 2
Time
0832-0857
0952-1017
1052-1117
1202-1227
1302-1327
1412-1437
1512-1537
1612-1637
1717-1742
1807-1832
1907-1932
2007-2032
Vmt>
Nm>
0.0270
0.0266
0.0263
0.0286
0.0284
0.0275
0.0278
0.0323
0.0289
0.0296
0.0298
0.0276
(std)
(dscf)
(0.952)
(0.941)
(0.930)
(1.01)
(1.002)
(0.972)
(0.982)
(1.14)
(1.022)
(1.046)
(1.053)
(0.973)
g/NrrP
0.072
0.051
0.091
0.062
0.061
0.087
0.075
0.067
0.062
0.088
0.095
0.088
(10*
Ib/dscf)
(0.045)
(0.032)
(0.057)
(0.039)
(0.038)
(0.054)
(0.047)
(0.042)
(0.039)
(0.055)
(0.059)
(0.055)
S02,
ppm
27.4
19.2
34.5
23.7
23.2
32.8
29.2
25.6
24.0
33.6
36.2
33.7
ng/J
63.2
43.4
78.6
54.6
52.4
67.9
64.5
55.4
57.2
80.8
82.5
68.8
(ib soy
1fj6 Btu)
(0. 147)
(0.101)
(0. 183)
(0. 127)
(0. 122)
(0. 158)
(0. 150)
(0. 129)
(0. 133)
(0. 188)
(0. 192)
(0. 160)
%02
14.6
14.4
14.5
14.5
14.5
13.9
14.2
14.2
14.9
14.9
14.6
13.9
S02,
ppm
26.6
39.2
40.2
29.0
29.2
33.1
35.3
34.1
20.1
36.3
34.6
37.4
ng/J
56.7
72.6
103.6
78.2
61.5
67.0
83.8
64.5
44.3
71.3
81.7
83.4
(Ib SO2/
1& Btu)
(0. 132)
(0. 169)
(0.241)
(0. 182)
(0. 143)
(0. 156)
(0. 195)
(0. 150)
(0. 103)
(0. 166)
(0. 190)
(0. 194)
%02
13.7
12.6
12.8
15.2
13.6
13.3
12.7
12.8
13.9
13.1
14.4
14.0
a Emission results based on use of 0.001
b Vm — metered volume (dry basis).
                          N barium perchlorate.
Tab/a 4.    30-Day Summary of SO2 Concentrations and Scrubber Efficiency
           March-April 1981
Hours
Date CEM Data
March 4
March 5
March 6
March 7
March 8
March 9
March 10
March 1 1
March 12
March 14
March 15
March 20
March 21
March 22
March 24
March 25
March 26
March 27
March 28
March 29
March 30
April 2
April 3
April 4
April 5
April 6
April 7
April 8
April 9
April 10
Mean
Maximum
Minimum
STD DEV
% STD DEV
24
18
21
23
19
20
20
19
18
18
22
21
19
23
22
18
21
21
23
19
18
24
21
22
22
22
22
23
22
23





S02lnlet SO2 Outlet
lb/1& Btu ng/J Ib /10ft Btu ng/J
4.00
3.10
4.11
3.82
4.16
4.17
4.88
4.37
4.45
6.19
5.21
4.95
5.22
4.64
5.48
4.97
6.15
4.85
4.52
6.43
5.38
4.83
5.07
4.79
5.27
5.15
5.40
5.50
6.16
5.06
4.94
6.43
3.10
0.75
15.2
1719.8
1332.9
1767.1
1642.4
1788.6
1792.9
2098.2
1878.9
1913.3
2661.4
2240. 1
2128.3
2244.4
1995.0
2356. 1
2136.9
2644.2
2085.3
1943.4
2764.6
2313. 1
2O76. 7
2179.9
2059.5
2265.9
2214.3
2321.7
2364. 7
2648.5
2175.6
2125.1
2764.6
1332.9
323.1
15.2
0.30
0.14
0.24
0.30
0.37
0.27
0.27
0.21
0.22
0.45
0.30
0.32
0.15
0.25
0.55
0.32
0.32
0.29
0.43
0.61
0.36
0.14
0.13
0.18
0.33
0.19
0.17
0.21
0.34
0.16
0.28
0.61
0.13
0.12
41.3
129.0
60.2
103.2
129.0
159.1
116.1
116.1
90.3
94.6
193.5
129.0
137.6
64.5
107.5
236.5
137.6
137.6
124.7
184.9
262.3
154.8
60.2
55.9
77.4
141.9
81.7
73.1
90.3
146.2
68.8
122.1
262.3
55.9
50.4
41.3
Eff
%
92.5
95.5
94.2
92.1
91.1
93.5
94.5
95.2
95.1
92.7
94.2
93.5
97.1
94.6
90.0
93.6
94.8
94.0
90.5
90.5
93.3
97.1
97.4
96.2
93.7
96.3
96.9
96.2
94.5
96.8
94.3
97.4
90.0
2.1
2.2

-------
Table 5. Coal Composition8
(%, except as noted)

2/12
Sulfur 2.62
Carbon 73.06
Hydrogen 5.24
Oxygen 9.24
Nitrogen 1.58
Chlorine 0.19
Volatile
matter 41.65
Fixed
carbon 50.09
Ash 8.26
Heat value.
kJ/kg 31,410
(Btu/lb) (13,500)
Moisture 3.66

2/13 2/14
2.80 3.00
73.67 69.37
5.22 4.72
8.38 13.84
1.56 1.51
0.21 0.20

41.54 41.71

50.09 50.73
8.37 7.56

31,040 31,225
(13,340) (13,420)
3.57 3.81

2/1 6 2/1 7
1.62 2.51
76.23 74.71
5.11 5.26
7. 19 7.59
1.81 1.64
0.20 0. 18

37.47 38.61

54.49 53. JO
8.04 8.29

31,550 31,410
(13.560) (13,500)
3.70 2.34
Date 1981
2/24 3/2-6" 3/9-13" 3/16-20" 3/23-27"
1.64 2.86 3.55 2.85 2.70
74.29 71.48 72.19 74.98 72.61
5.30 5.37 5.19 5.37 3.64
9.06 7.76 7.72 7.83 11.77
1.74 1.54 1.56 1.65 1.54
0.14 0.18 0.12 0.16 0.09

37.18 38.99 39.08 40.82 40.01

54.85 50.20 51.25 52.02 52.34
7.97 10.81 9.67 7.16 7.65

31,690 30,250 30,510 31,620 31,010
(13,620)(13,000) (13,114) (13,590) (13,328)
2.02 8.62 7.92 9.35 6.99

3/30-4/3" 4/6-1 Of
2.73 2.22
74. 1 3 75.50
5.33 5.61
9.78 8.99
1.49 1.67
0.09 0. 12

40.58 40.93

52.97 53.18
6.45 5.89

31,240 32,470
(13.427) (13.955)
6.35 4.26
aDry basis except for moisture.
^Composite.




Table 6. Adipic Acid, Limestone, and Coal Usage

Date
11981)
February 20
21
22
23
24
25
26
27
28
March 1
2
3
4
5
6
7
8
9
10
11
12
13
14
15
16
17
18
19
20
21
22
23
24
25
26
27
28
29
30
31
pril 1
2
3
Average
adipic acid feed.
kg/h (Ib/h)*






3.63 (8)
3.63 (8)
1.81 (4)
1.81 (4)
3.63 (8)
2. 72 (6)
6.35 (14)
2. 72 (6)
4.54 (10jc
5.44 (12)c
3.63 (8)c
4.54 (10)c
3.63 (8)
3.63 (8)
3.63 (8)
2.62 (6)
4.08 (9)
4.08 (9)
4.54 (10)
3.63 (8)
7.26 (16)'
4.54 (10)
7.26 (16)c
6.35 (14)c
1.81 (4)d
2. 72 (6)
3.63 (8)
4.54 (10)
3.63 (8)
4.54 (10)
4.54 (10)
3.63 (8)
2.27 (5)^
OfOJf
6.35 (14)c
5.44 (12)
3.63 (8)
Average
limestone feed.
kg/h (Ib/hp



261 (575)
281 (619)
331 (729)
319 (702)
325 (716)
311 (686)
321 (707)
327 (720)
341 (752)
362 (798)
372 (820)
360 (793)
388 (854)
387 (853)
370 (814)
347 (765)
350 (771)
353 (778)
337 (742)
331 (728)
332 (731)
311 (686)
220 (489)
246 (542)
320 (704)
404 (890)
391 (861)
318 (700)
218(479)
236 (520)
298 (656)
285 (627)
270 (595)
262 (576)
213(468)
184 (405)<>
0(0)'
292 (644)
212(467)
198 (435)
Mg (tons)
of coal
used/day
85.0 (77. 1)
90.3 (81.9)
92.7 (84.0)
112.1 (101.6)
126.6(114.8)
127.8(115.9)
113.4(102.8)
130.4(118.2)
113.5(102.9)
124.6 (113.0)
108.6(98.5)
106. 1 (96.2)
100.8(91.4)
112.6(102.1)
132.0(119.7)
131.4(119.1)
138. 1 (125.2)
123.1 (111.6)
121.1 (109.8)
99.9 (90.6)
94.6(85.8)
97.5(88.4)
102. 1 (92.6)
101.1 (91.7)
112.3(101.8)
133.2 (120.8)
118.5 (107.4)
136.4 (123. 7)
127.1 (115.2)
113.2(102.6)
99.2 (89.9)
103.2 (93.6)
98.8(89.6)
98.5 (89.3)
94.2 (85.4)
97.9(88.8)
95. 1 (86.2)
78.4(71.1)
69.4 (62.9)
79.9(72.4)
71. 1 (64.5)
76. 1 (69.0)
60.8(55.1)















































-------
  Table 6.   (continued)
Date
11981)
4
5
6
7
8
9
10
Average
adipic acid feed,
kg/h (lb/h>»
3.63 (8)
1.81 (4)1
4.54 (10)
4.54 (10)
2. 72 (6)
2.72(6)
2.27 (5)
• Average
limestone feed,
kg/h (Ib/hp
218(480)
239 (526)
276 (608)
225 (496)
207 (455)
203 (447)
212 (467)
Mg (tons)
of coal
used/day
60.9 (55.2)
74.2 (67.3)
68.1 (61.7)
68.4 (62.0)
66.2 (60.O)
63.4 (57.5)
74.2 (67.3)
  "24-hour basis.
  t>Based on hours of feed.
  cAdipic acid was dumped in the thickener.
  ^Vibrator was turned off. Adipic acid feeder plugged.
  eScrubber was bypassed at 1940 because the thickener was
   adipic acid feeds were turned off at that time.
  'The scrubber was still off-line.  It was restarted before 8 a. m.
                      plugged.  Limestone and

                      on April 1.
     P. A. Clarke, R. W. Gerstle, D. S. Henzel, K. W. Mason, andS. R. Sabatiniare with
       PEDCo Environmental, Inc., Cincinnati, OH 45246.
     J. David Mobley is the EPA Project Officer (see below).
     The complete report, entitled "The Adipic Acid Enhanced Flue Gas Desulfurization
       Process for Industrial Boilers: Volume  1. Field Test Results." (Order No. PB
       83-144 774; Cost: $32.50. subject to change) will be available only from:
             National Technical Information Service
             5285 Port Royal Road
             Springfield, VA 22161
             Telephone: 703-487-4650
     The EPA Project Officer can be contacted at:
             Industrial Environmental Research Laboratory
             U.S. Environmental Protection Agency
             Research Triangle Park,  NC 27711
United States
Environmental Protection
Agency
Center for Environmental Research
Information
Cincinnati OH 45268
Postage and
Fees Paid
Environmental
Protection
Agency
EPA 335
Official Business
Penalty for Private Use $300
          PS   0000329
                                           AGENCV

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