625/2-79-022 v>EPA United States Environmental Protection Agency Industrial Environmental Research Laboratory Research Triangle Park NC 27711 Technology Transfer Capsule Report Bahco Flue Gas Desulfurization and Particulate Removal System ,?' •*- ,1* ------- Technology Transfer EPA 625/2-79-022 Capsule Report Bahco Flue Gas Desulfurization and Paniculate Removal System July 1979 This report was developed by the Industrial Environmental Research Laboratory Research Triangle Park IMC 27711 ------- Scrubber circulating pump and piping ------- 1. Introduction and Summary This capsule report has been prepared as an aid in solving one of today's vitally important technological concerns the selection and use of fuel for industrial-size steam generating units and other fuel-burning equipment. Reduced availability of natural gas supplies, increased cost of low sulfur oil, and pollution problems generally associated with coal currently present operators of boiler installations with a question: What is the best technique for compliance with particulate and sulfur dioxide regulations? The flue gas desulfurization (FGD) technology described herein permits any fuel, including high sulfur oil or coal, to be burned in conventional equipment in a manner that is both cost effective and environmentally acceptable. In September 1974, the U.S. Air Force (USAF) awarded a contract to Research-Cottrell (R-C) to erect an SC>2 and particulate emission control system at the central heat plant of Rickenbacker Air Force Base (RAFB) near Columbus, Ohio. The equipment chosen was an R-C/Bahco scrubber (module size 50) based on technology developed by A B Banco in Sweden. This unit accomplishes both S02 and particulate removal The R-C/Bahco system has been used on many foreign oil-fired industrial boilers since 1969. The installation at the Rickenbacker facility is the first application of the system on a coal-fired industrial boiler. A second contract, sponsored by the U.S. Environmental Protection Agency (EPA), was awarded to Research-Cottrell in April 1975. The key provision of this program was to characterize the R-C/Bahco scrubbing system installed at RAFB in terms of its performance, reliability, and economics for S02 and particulate control on industrial coal-fired plants. The R-C/Bahco system was started up in March 1976; the Characteriza- tion Program was started a month later and was completed in June 1 977. Final acceptance of the system by the USAF followed in September 1977, at the end of a 1-year operating cost guarantee period. ------- The Characterization Program demonstrated that the R-C/Bahco scrubbing system is capable of controlling both paniculate and sulfur dioxide emissions from the combustion of high sulfur (2 to 4 percent) midwestern coal. The following salient data were obtained during the program: • Paniculate emissions were reduced to as low as 0.15 lb/106Btu(0.27g/106cal). • Sulfur dioxide emissions were reduced to as low as 0.1 lb/106 Btu (0.18 g/106 cal) with lime reagent, and as low as 0.6 lb/106 Btu (1.1 g/106 cal) with limestone. • Operating costs, exclusive of capital charges, were $5.28/ton of coal burned when using lime, including $0.21 maintenance costs. • Waste product properties relative to dewatering, handling, and disposal were found to be similar to those measured for other FGD waste products. • Operation of the system required less than 2,000 man-hours per year. System availability above 95 percent is projected. • No significant buildup of scale or solids occurred in the scrubbing system during the test program. Bin activator, feeder, and lime slaker ------- 2. The FGD System The R-C/Bahco facility operating at RAFB is a calcium-based throwaway FGD and paniculate removal system. Either pebble lime (CaO) or ground limestone (CaCOs) can be used for SC>2 removal to produce mixtures containing calcium sulfite (CaSOs), gypsum (CaSCU), and fly ash. The overall chemical reactions for the respective reagents are shown in Table 1. The scrubbing system comprises the following major components: • Flue-gas-handling equipment • R-C/Bahco scrubber • Reagent-handling and -storage equipment • Sludge disposal equipment The entire FGD system (Figure 1) is served by a centrally located control room and is operated, part time, by heat plant personnel. Flue-Gas-Handling Equipment The flue-gas-handling equipment includes a flue gas header, bypass stack, mechanical collector, and booster fan. Flue gas from as many as eight stoker-fired hot water generators—up to 108,000 actual ftVmm (51 m3/s)—passes into the header and mechanical collector where coarse paniculate matter is removed before it enters the booster fan and scrubber. Removing paniculate minimizes erosion of the fan and other scrubber components and reduces the amount of wet solids handled by the scrubbing system. The ash is disposed of via the existing ash-handling system. A bypass stack in the carbon steel flue gas header serves two purposes: it serves as a fail-safe emergency bypass, and it permits air to enter the system at low loads to maintain gas velocity through the mechanical collector and scrubber to maximize collection efficiency. Gas Flow As shown in Figure 2, the R-C/Bahco scrubber, which is fabricated from 316L stainless steel, is a two-stage inverted venturi unit specifically designed to operate with slurries containing calcium sulfite, calcium sulfate (gypsum), calcium carbonate, calcium hydroxide, and fly ash. All of the internal gas flow passages are large, unobstructed, and well irrigated with circulating slurry or makeup water to essentially eliminate the possibility of serious plugging problems. Hot flue gas from the booster fan enters the first stage, where it impinges on the surface of the slurry, creating a cascade of droplets that it carries into the throat of the lower venturi. The droplets, containing SC>2 scrubbing reagent, cool the gas to its saturation temperature, absorb sulfur dioxide, and trap paniculate Table 1. Chemical Reactions for Lime and Limestone in SC>2 Removal Reagent Reaction Lime Limestone CaO + HyO CaCOj + SOy - —• — >- Ca{OH)2 ». CaSO -j + CO'i ------- Thickener Reagent system module Reagent storage Reagent feeder and slaker Lime or limestone conveyor Unloading station — Overflow to lime- dissolving tank Bypass Flue makeup gas stack^ from heat plant Reagent-dissolving Second stage tank pump Mill pump To fly ash disposal Figure 1. R-C/Bahco Scrubber System matter. Above the first venturi, the gas stream is turned downward by the bottom of the pan in the second stage venturi causing most of the droplets to fall out. In the second stage, or upper venturi, the process of impinging the gas stream on the surface of a slurry is repeated. Here the gas/droplet mixture passes up through the throat of the upper venturi where final S02 absorption and paniculate removal are accomplished. A cyclonic mist eliminator above the upper venturi imparts a spinning motion to the gas stream, causing the droplets to move toward the wall where they coalesce and drain from the scrubber. From the mist eliminator, clean gas, which is not reheated, enters the surrounding atmosphere via the stack. Slurry Flow Two techniques of handling slurry flow in the system are used to eliminate or minimize the plugging and erosion problems often associated with calcium-based FGD systems: maintaining essentially constant slurry flow rates through the scrubber, and eliminating turndown in slurry bleed streams by operating in an ------- Schedule Gas flow Slurry flow Sludge removal Slowdown valve-/ v To reagent dissolver* Stack Manhole Platform Man door Platform Platform stage drop collector Ground level Figure 2. R-C/Bahco Scrubber ------- on-and-off mode with water flushing after slurry flow is interrupted. Slurry flows by gravity from top to bottom in the scrubber, counter- current to the gas flow. Slurry from the reagent dissolver (which is also of 316L stainless steel) contains makeup reagent—either lime or ground limestone. The slurry enters the pan in the upper venturi. Slurry level in the pan determines the upper venturi pressure drop; the level is set by adjusting a weir in the level tank located outside the scrubber. Slurry streams from the mist eliminator and the pan are combined in the level tank before flowing by gravity to the mill under the lower venturi, where another level tank is used to set the pressure drop in the lower venturi. Part of the slurry collected in the area between the upper and lower Venturis, the part that has contacted the gas stream twice, flows by gravity to the sludge disposal system. In the first-stage level tank this slurry is combined with overflow from the mill and is returned to the reagent dissolver. More reagent is added in the dissolver before the slurry is recycled to the upper venturi. The fluid mill is powered by an external pump and is used to grind coarse limestone or other large particles in the system. First-stage venturi, showing gas inlets and makeup water spray manifolds Reagent-Handling and -Storage Equipment The reagent system installed at RAFB is capable of handling both 0.75-inch (1.9-cm) pebble lime and 200-mesh ground limestone. Primary components include truck-unloading equipment, a steel silo with 3 weeks' storage capacity at winter load conditions, a weigh belt feeder, and a lime slaker. The silo, feeder, slaker, and reagent- dissolving tank are integrated into a single module to minimize materials handling, supports, and space requirements. Lime or limestone drops directly out of the silo into the feeder-slaker and overflows into the reagent-dissolv- ing tank directly under the slaker. Sludge Disposal Equipment Calcium sulfite, gypsum, and fly ash collected in the scrubber are concentrated from 10 percent to approximately 40 percent solids (by weight) in a thickener. The overflow from the thickener is returned by gravity to the reagent-dissolving tank. The underflow from the thickener is pumped underground to a hypalon-lined storage pond. ------- 3. The Test Program The R-C/Bahco FGD system test program, carried out at RAFB between March 1976 and June 1977, incorporated the following categories: • Material balance • Lime reagent process variable • Lime reagent verification • Particulate collection efficiency • Limestone reagent process variable • Sludge characterization • Scrubber reliability monitoring Material balance tests were conducted to establish the range of operating conditions over which the R-C/Bahco scrubber could be operated and to verify performance at design conditions by completing material balances. Maximum and minimum gas flow rates, pressure drops, and slurry circulation rates were determined and preliminary SOa and the paniculate performance data at the limits of the system's capabilities were obtained. The system was operated at the design gas rate of 50,000 stdftVmin (25 normal m3/s) and complete material balances on calcium, sulfur, and total solids were performed. Statistically designed lime process variable tests helped to establish the quantitative effect of the following process variables on SC>2 removal: gas flow rate, first- and second-stage pressure drops, mill and second-stage slurry rates, lime.SO2 stoichiometric ratio, slurry inventory, and slurry solids concentration. Lime reagent verification tests were undertaken to verify the results obtained in the lime process variable tests, and to determine the effect of very dilute scrubber slurry (2 percent solids) on system performance. Particulate collection efficiency tests were a continuation of the paniculate tests initiated during the earlier sampling phase. Relationships were determined between system variables, including particle size distribution and paniculate removal efficiency. Limestone process variable tests were completed using the same statistically designed test plan used for lime. The effect of system variables on SOa removal efficiency and reagent use was determined. Sludge samples generated at RAFB were tested to determine dewatering, transport, and disposal characteristics (sludge characterization). Samples of sludge from lime as well as limestone scrubbing were tested. The R-C/Bahco system was monitored from March 1976 to June 1977, to document its operating and maintenance history and to obtain data for a cost analysis. Data were gathered on reagent, coal, water, and power consumption as well as on operating and maintenance labor requirements. Throughout the test program samples were taken of slurry, flue gas, lime, limestone, and coal, often in duplicate, for chemical analyses, paniculate loading, and particle size distribution. A field analytical laboratory was established, and especially developed and highly efficient test methods using thermogravimetric analysis were employed extensively. ------- 4. Test Results Capacity/Material Balance Tests Performance of the size 50 R-C/Bahco scrubber at RAFB is measured by its ability to handle variations in system operating parameters while reducing S02 and particulate emissions to the limits allowed by the applicable regulations, without exceeding the capacity of the system. Regulations applicable to RAFB limit SOa emissions to 2.2 lb/106 Btu (3.96 g/106 cal) and particulate to 0.16 lb/106 Btu (0.29 g/106 cal). Table 2 lists maximum, minimum, and optimum operating levels determined for the system at RAFB. The cost of reducing emissions to meet requirements will be minimized at optimum operating levels. Lime Tests The SC>2 removal capabilities of the R-C/Bahco system using pebble lime were characterized in two steps. First, a series of screening tests determined the effects of slurry rates, gas rate, venturi pressure drops, slurry density, system volume, and lime stoichiometry on SC>2 removal. Tests results indicated that lime stoichiometry—the ratio of lime feed in the system to 862 in the flue gas—was the only variable controlling SC>2 removal as long as the system was operated within the limits outlined in Table 2. A second group of tests, in which the effects of the gas flow, slurry rates and slurry density were determined, confirmed the initial findings that stoichiometry alone controlled S02 removal. Results of these verification tests are shown in Figure 3 The figure also shows that lime use is essentially 100 percent—that is, no excess lime is needed—up to 90 percent SC>2 removal. Figure 4 illustrates system performance when S02 removal is above 90 percent—that is, when SC>2 emissions at RAFB were reduced below 0.6 lb/106 Btu (1.08 g/106 cal). The figure indicates that over 98 percent of the S02 corresponding to 0.1 Ib S02/106 Btu (0.18 g S02/106 cal), can be Table 2. R-C/Bahco Scrubber Operating Levels Variable Gas rate (actual ft3/mm) Slurry circulation rate (gal/mm) . . . Venturi pressure drop for each stage (inches H20) Slurry concentration (wt % solids) Reagent.SC>2 stoichiometry (moles reagent moles SC>2, based on inlet SOa levels) Lime Limestone S02 removal efficiency (percent) Lime Limestone S02 emission (lb/106 Btu) Lime Limestone Particulate emission (lb/106 Btu) Minimum 35,000 1,500 6 2 045 055 45 40 3.7 40 02-03 Maximum 55,000 3,000 12 25 1 05 1 2 98+ 85 01 1 0 014 Optimum 40,000-50,000 2,300 7-10 10 07 075 70 70 20 20 0 16 ------- achieved with a stoichiometry of 1.1—that is, 10 percent excess lime. The S02 emission rates shown in Figure 4 are well below the required 2.2 lb/106 Btu (3.96 g/106 cal) and the guarantee level of 1.0 lb/106 Btu (1 8 g/106 cal). From the lime tests it is concluded that lime:S02 stoichiometry is the controlling factor in determining S02 removal efficiency. Virtually any desired S02 removal efficiency can be achieved when lime is used in the R-C/Bahco scrubber, simply by adjusting the lime:S02 stoichiometry. Lime use approaches 100 percent at stoichiometric ratios up to about 0.9. At stoichiometric ratios up to 1.1, producing up to 99 percent removal, lime use is above 90 percent. Because most S02 regulations for industrial boilers permit emissions in the range of 1.0 to 2.0 lb/106 Btu (1.8 to 3.6 g/106 cal), lime, with its high removal capabilities, can be used to obtain offset credits in a nonattainment area to apply toward an expansion or new facility. No further capital expenditure need be made, because the R-C/Bahco system normally would be designed to handle lime as well as limestone, and switching from limestone to lime will increase the annual operating costs only by about 15 percent. Limestone Tests System performance with ground limestone was determined in a series of screening tests very similar to those used for pebble lime. These tests indicated that slurry circulation in addition to limestone stoichiometry controls S02 removal efficiency. < > o 100 80 60 40 20 RAFB Code requirement r?\° 02 04 06 Oi 1 0 1 2 1 4 LIME STOICHIOMETRY (moles lime per mole (S02) Figure 3. S02 Removal Efficiency as a Function of Lime Stoichiometry Hypalon-hned storage pond ------- Figure 5 shows the results of the tests and gives limestone use data. At a stoichiometry of 1.0 and slurry circulation of 2,300 gal/min (0.14 m3/s), slightly over 80 percent SC>2 removal is possible with 80 percent limestone use. A practical limit for limestone is 80 percent SOa removal, because higher removals result in substantial reductions in limestone use. Operation with limestone at RAFB produced sludge that contained much more gypsum than did operation with lime. That is, there was more oxidation of CaSOa to CaSO4. Table 3 shows an average gypsum (CaS04 • 2H20) and calcium sulfite (CaS03-1/2H20) content of 33 and 55 percent, respectively, when lime was used. The limestone slurry was almost completely oxidized and contained 78 percent sulfate and less than 1 percent sulfite. The comparison of average lime and limestone slurry analyses during similar boiler load periods listed in Table 3 indicates that the oxidation trend is probably attributable to the lower slurry pH encountered when using limestone, because all other operating conditions were essentially the same. Particulate Removal Efficiency Paniculate Removal Tests. Initial particulate removal tests on the R-C/Bahco scrubber, performed in March, April, and May of 1976, revealed the presence of substantial amounts of soot in the stack gas. The average particulate emission rate for these tests was 0.23 lb/106 Btu (0.42 g/106 cal). 2 5 £ 20 ID o £ 15 < tr 1 0 "J 05 RAFB EPA limit Guarantee emission rate 90% lime use 07 08 09 10 11 12 13 14 LIME STOICHIOMETRY (moles lime per mole S02) 1 5 Figure 4. Relationship Between SOa Emission Rates and Lime:SOa Stoichiometry Overall particulate removal averaged 93 to 94 percent. Ohio emission standards require an overall removal efficiency of 96 percent at a particulate inlet loading of 1.5 gr/stdft 3 dry (3.4 g/normal m3 dry) to achieve an emission rate of 0.16 lb/106 Btu (0.29 g/106 cal). Venturi pressure drops were increased to nearly double the design value of 7 inches (18 cm) H20 to reduce these emissions. Below approximately 18 inches (46 cm) H20 total pressure drop, particulate emissions increased rapidly. The amount of soot present in the flue gas at RAFB is higher than in other stoker-fired generators similar to the Rickenbacker boiler. The Air Force has undertaken an extensive program to upgrade the heat plant at RAFB. Data obtained during this test program contributed substantially to information used to plan the upgrading program, and so far the following modifications have been completed: • Installation of a new 60-Btu/h (18-Watt) generator to replace the two old units • Replacement of hot water distribution piping • Installation of flue gas oxygen monitoring equipment • Repair of firing air distribution equipment and fire box pressure controls in the generators ------- • Rebuilding mechanical collectors and induced draft fans on the generators • Replacement of burned out ledge plates, which regulate combustion air flow around the grates • Repair of traveling grates The problem with soot at RAFB points up a critical aspect of a successful emission control project—namely, that proper operation of all equipment, boilers as well as the scrubber, is essential to maintain satisfactory emission levels. Inadequate combustion or inadequate air can be as detrimental to emission control as improper scrubber operation. Slurry Entrainment and Gas Bypassing. During the particulate tests, two phenomena were observed when the system was operated above its capacity limits. The first, called entrainment, occurs at very low venturi pressure drops—that is, under 6 inches (15 cm) h^O involves small droplets of slurry carrying through the second-stage mist eliminator and out the stack. The second, called bypassing, is characterized by pulsations in the gas flow through the scrubber; the result is low collection efficiency in all particle size ranges. The second phenomenon takes place when relatively high pressure drops—that is, 12 inches (30 cm) H20 or more in either venturi—are coupled with slurry flows under 150 gal/min (0.01 m3/s) to the scrubber. Conclusion. The particulate removal efficiency of the R-C/Bahco scrubber is comparable to that of low energy venturi scrubbers for particles larger than 1 Mm, and appears to be better for particles smaller than 1/im. In an R-C/Bahco scrubber, the second stage is the primary collector of fine particles. Slurry carryover and 100 90 80 c <" in o /U LLJ u 60 50 0 40 30 20 10 02 04 06 08 10 12 14 16 18 STOICHIOMETRY RATIO Figure 5. S02 Removal Efficiency as a Function of Limestone:S02 Stoichiometry Table 3. Lime and Limestone Slurry Analyses Slurry solids CaS04 2H20 CaSOa V2H20 CaCOs MqCO-i . Acid insolubles Lime slurry (wt%) 334 54 5 3 7 46 Limestone slurry (wt%) 77 5 1 0 17 3 08 3 4 Total 962 1000 ------- gas bypassing limit paniculate Table 4. collection in an R-C/Bahco ^ T scrubber operated outside the Dewater.ng Test Results levels shown in Table 1. Particulate emissions from stoker-fired coal-burning levels required by regulatory • .r '. ' Settling agencies if excessive soot u formation is prevented. Centrifuge Sludge Characterization Filter leaf A series of scrubber sludge Slurry type / Lime \ Limestone3 I Lime ... < Lime \ Limestone I Lime / Lime \ Limestone Feed solids (wt%) 162 167 167 263 384 374 246 41 5 374 Final solids (wt%) 44 58 58 51 56 65 58 59 74 Rate at 35 percent solids 22 Ib/d/ft2 1 64 Ib/d/ft2 578 Ib/d/ft2 70 Ib/h/ft2 124 Ib/h/ft2 64 Ib/h/ft2 characterization tests was carried out at the Research-Cottrell laboratories to: • Determine scrubber sludge dewatering characteristics • Evaluate transportability of dewatered sludge • Determine physical/structural properties of dewatered sludge • Measure sludge leachate properties Slurry Dewatering. A series of settling, centrifuge, and filter leaf tests was run on lime and limestone slurry samples. The results are summarized in Table 4. The settling tests showed that limestone slurries settle more rapidly and produce denser settled layer than lime slurries. Flocculation improved the settling of limestone slurries, but not that of lime slurries. aWith 5 ppm flocculant Table 5. Sludge Leachate Analysis Analysis IDS (mg/l) S04 (mg/l) . . . . COD (mg/l) Cl (mg/l) . . . Pb (ppb) . . Cd (ppb) Cr (ppb) Hg (ppb) Lime leachate 2 960 1 8106 8 4 72 52 <100 ... < 1 0 .... 50 <25 Limestone leachate 2 760 1 613 1 68 4804 <100 <10 50 <25 ------- The centrifuge tests indicated that final cake density increased as the solids concentration in the feed was increased, and that limestone slurries produced higher cake densities than did lime slurries. Filter leaf tests showed that limestone slurry filtration rates were significantly lower than lime slurry rates. However, limestone again produced a denser cake. Leachate Tests. Leachate tests were performed on samples of lime and limestone sludges. The results are listed in Table 5. Leachate compositions from lime and limestone sludges are essentially the same. Total dissolved solids (TDS) in the range of 2,500 to 3,000 mg/l and sulfate levels of 1,600 to 1,800 mg/l indicate that the leachates were saturated with respect to CaSC>4. Both sulfites in the sludge and organic matter in the fly ash contribute to the chemical oxygen demand (COD) levels observed. Although the chloride level in the lime leachate is somewhat higher than the limestone leachate, the other trace elements are present in similar concentrations in both leachates. The constituents found in these leachates are similar in type and concentration to those reported in other studies. If a disposal site is placed so as to avoid infiltration of leachate into ground water, and if sludge and soil cover are placed properly to avoid excessive contamination of runoff, leachate from these sludges will not present an environmentally unacceptable disposal problem. First-stage level tank ------- 5. Operating Experience Since startup in March 1976, the R-C/Bahco system has performed well in all areas essential to successful FGD, including: S02 removal Paniculate removal Scrubber reliability Minimal routine maintenance Moderate operating costs Ease of operation During the test period of about 11,000 hours, the scrubbing system operated for 6,194 hours. The operation is summarized in Figure 6. It is of interest that from December 1976 to February 1977 (when severe winter weather was encountered), no outages resulted from failure of auxiliary equipment. There were a few brief shutdowns caused by frozen air and water lines during this period, but system availability was over 95 percent. Downtime is summarized in Table 6. This table shows the amount of time required to obtain parts as well as the actual time for repair work. Spare parts were not kept on hand during the test period, and this resulted in substantial unnecessary downtime. Since completion of the test program, a full supply of spares has been procured. Table 6 also shows that booster fan repair time accounted for 90 percent of the downtime caused by repairs. The booster fan operates on the inlet side of the scrubber, downstream from the mechanical collector, and handles only hot dry flue gas with moderate amounts of fine fly ash. Modifications to the fan wheel and bearings, completed in May 1977, have eliminated the recurring failures associated with this piece of equipment. Total downtime, exclusive of fan repairs and procurement, was 1,845 hours, or 17 percent of the test period. During routine operation, the system availability should be over 95 percent, based on the factors observed during the test program. Scrubber inspections were an integral part of the program to monitor scrubber performance. A thorough internal inspection was made in April 1976, approximately 1 month after startup. A followup inspection was made 2 months later, with subsequent inspections during outages up to the end of the test program in June 1977. These inspections confirmed the effectiveness of the water makeup system in keeping key areas of the scrubber clean. ------- Accumulations of solids were detected at seven locations within the scrubber (Figure 7). Accumulations in four areas—1, 5, 6, and 7—had no impact on scrubber performance. Problems of solids buildup in Areas 2, 3, and 4 were easily corrected, as follows: In the first few months after startup, the first-stage venturi overflowed into the inlet manifold. Area 2, resulting in an accumulation of dried slurry in the bottom of that area. Subsequent investigation revealed that operation of the first-stage at pressure drops above 12 inches (30 cm) H20 coupled with a second-stage slurry pumping rate more than 50 percent higher than the design rate of 2,600 gal/mm (0.16 m3/s), caused flooding when the gas flow was reduced below 35,000 stdftVmin (17 normal m3/s) or the booster fan was shut down. This problem was eliminated by decreasing the speed of the slurry pump to reduce the flow to design levels, and by adding an interlock to stop the pump when the booster fan is shut down. The accumulated material was removed during subsequent heat plant outages. Areas 3 and 4 were affected twice during the test by accumulations of a coarse sandy material. The first incident, which occurred shortly after startup, was caused by inadequate removal of grit from the lime slaker. The material in the pan was removed and the slaker was readjusted to eliminate the problem. The second accumulation took place during the winter of 1976-77 when the air lines, which activated the blowdown valves on the first- and second-stage level tanks, froze and rendered these valves inoperative. II III I U t fit lnsta" 1 Scrubber Replace slurry Scrubber Replace slurry sludge 1 startup pump lining inspection pump lining thickener rake Mar Apr May 1976 II II 4 t ReplaCe Correct )orque fan vibration limiter July Aug Sept 1976 June II III Repair sludge and slurry lines Oct. I.I Install improved J^'3,06 booster fan bearing blowdown valves Nov Dec Jan 1976/1977 .II , ,l t \ ft Replace ' Inspection Repair and Replace water booster and grit modification slaker pump bearing removal of fan wheel motor Mar. Apr May 1977 Feb Scrubber 1 1 operabihty 1 1 Boiler 1 I shutdown 1 1 Figure 6. Downtime Related to Auxiliary Equipment Table 6. Downtime Summary Hours Percent Booster fan Thickener Slurry pump Water booster pump Lime slaker . . Modifications Routine maintenance Loss of utilities Miscellaneous . .... Total Procurement 514 471 252 190 122 56 1 605 Repairs 2 252 8 18 16 11 58 2 363 Downtime 2 766 479 270 206 133 388 139 1 16 1 14 4 61 1 period 25 1 4 4 2 5 1 9 1 2 3 5 1 3 1 1 0 9 41 9 ------- The results of this part of the test program demonstrated that there are situations that can result in deterioration of scrubber performance, including: • Infiltration of grit into the system through the lime slaker • Inadequate operation of the scrubber blowdown valves • Slow accumulation of solids in the straightening vanes in the stack The infiltration of grit can be kept to a minimum by paying close attention to the operation of the lime slaker grit removal circuit. The blowdown valves should be operated two to four times a shift, depending on scrubber load, to avoid accumulations of solids in the slurry outlets. The straightening vanes at the base of the stack, which serve only to minimize spin in the gas stream leaving the scrubber, may accumulate some material and should be checked twice a year. The possibility of accumulations taking place can be minimized by operating the scrubber within the limits outlined in Section 3 to avoid slurry carryover. Obviously, elimination of the vanes would prevent the problem entirely, but accurate outlet particulate sampling would then be difficult. The RAFB operating experience indicates that there are no significant problems related to the accumulation of solids in the R-C/Bahco system. The scrubber can tolerate substantial accumulations of solids resulting from external operating problems before performance is adversely affected. Any deterioration in performance that does occur is gradual and can be rectified at a convenient time. Stack Manhole 7 6 *- J Platform Mist eliminator Man door Manhole Ground level Platform Platform stage drop collector * Water makeup system Figure 7. R-C/Bahco Scrubber Module ------- Lime delivery truck with R-C/Bahco scrubber and lime bin in background ------- 6. Economics Compliance with air pollution control regulations can be achieved in several ways. The one frequently chosen today is switching to a fuel such as low sulfur oil that does not require emission control equipment. This choice is often based on an economic evaluation that proves it cost-effective. Table 7 summarizes data gathered on costs during the test program at RAFBa. During the 14-month test period, flue gas from the combustion of 27,216 tons (24,742 Mg) of coal, which averaged 2.5 percent sulfur, was treated by the scrubbing system. The total operating cost—including utilities, chemicals, and labor—was $5.07/ton of coal burned. Maintenance costs were $0.21/ton including labor and materials. Sludge disposal cost is $0.45/ton of coal burned, calculated in terms of the installed cost of the pond and an anticipated 10-year life. The turnkey cost of the RAFB installation was $2.25 million, including a new substation and additional equipment, controls, and instrumentation necessary for the EPA test program. Current costs for R-C/Bahco turnkey systems (Figure 8) are $1.3 million to $3.7 million. Figure 9 illustrates the capacities of the various size systems. The system installed at RAFB is capable of treating flue gas from a 180,000-lb/h (23-kg/s) steam boiler. Table 8, based on the cost data collected at RAFB, summarizes the annual operating costs including normal overheads and capital charges for an industrial 180,000-lb/h (23-kg/s) steam plant operating at 75 percent of capacity. The 1979 cost of low sulfur oil is approximately $20 to $22/barrel, or about $87 to $96 for energy equivalent to that contained in 1 ton (0.91 Mg) of coal: 25 Btu x 106 (26.4 kJ x 106). In the case outlined in Table 8, there would be an annual fuel saving of between $3,400,000 and $4,000,000, which could be applied to coal-handling and emission control equipment if coal at $30/ton were burned instead of low sulfur oil. The R-C/Bahco system is designed specifically for industrial-size fossil-fuel-burning applications that require combined S02 and particulate removal. The system at RAFB handles SOa and particulate from the combustion of midwestern high sulfur coal, 12,200 Btu/lb (28,377 kJ/kg), 6 percent ash, 3.5 percent sulfur. Other units, listed in Table 9, have been operating successfully since 1969 on oil-fired boilers with S02 concentrations up to 4,000 ppm. Basically, the R-C/Bahco system can economically reduce 562 particulate emissions from the combustion of coal and high sulfur oil, or emissions from certain other sources, to levels low enough to satisfy applicable environmental regulations. The R-C/Bahco system can be used successfully for emission control for almost any installation, where the SC>2 concentration does not exceed 6,000 ppm and most of the particulate to be collected is above 1 ^im. a1978 is the base year for costs unless otherwise indicated. ------- Table 7. RAFB Operating Cost Summary Item Units Cost (S) Per unit Total Power Booster fan 3,065,000 kWh Auxiliary equipment 602,500 kWh Water Potable water 4,448,120 gal Well watej > Chemicals Lime Limestone Labor Operating labor Supervision (25% of operating labor estimate) 1,768,700 gal 721 tons 130 tons 0 024/kWh 0 024/kWh 036/1,000 gal 40 35/ton 1272/ton 1,860 man-hours 7 52/man-hour Total . 73,560 14,460 1,601 29,092 1,654 13,987 3,497 137,851 40r- 35 30 « 25 (ft 8 20 1 5 1 0 05 0 I J I 10 20 30 40 50 60 70 80 90 100 FLUE GAS FLOW RATE (1,000 stdftVmm) Figure 8. R-C/Bahco Capital Costs ------- 100 00 00 D cc o in O o < CO X CJ RAFB flow rate Average Maximum Suggested operating range 10 20 30 40 50 60 70 80 90 FLUE GAS FLOW RATE (1,000 stdftVmin) 100 110 120 Figure 9. R-C/Bahco Scrubber Capacities Table 8. Annual Operating Costs Item Units Cost (S) Per unit Total Power Water Chemical (limestone) Sludge dewatering3 Operating labor Supervision of labor Maintenance labor and materials General overhead (75% of labor man-hour costs) Depreciation (10-year straight line) Taxes and insurance 3 5 million kWh 6 million gal 4,440 tons 2,200 man-hours 500 man-hours 0 024/kWh 036/1,000 gal 1272/ton 84,000 2,160 56,480 800/man-hour 17,600 1000/man-hour 5,000 12,600 - 17,300 - 225,000 — 45,000 Total 465,140 a Included in other costs Note —Installed cost = $2 25 million Coal consumption = 60,000 tons at 3 percent sulfur + 70 percent S02 removal Cost per ton of coal = $7 50 ------- Table 9. R-C/Bahco Particulate/S02 Removal Systems Company and location Rickenbacker Air Force Base . . . Columbus OH Kino Ura Utility Japan Kanegafuchi Chemical Takasago, Japan Stora Kopparberg .... . . . Grycksbo, Sweden Osaka City ... Osaka, Japan Central Glass Company .... Sakai, Japan Taio Paper Company . lyomishima, Japan Yahagi Iron Works Nagoya, Japan Hiroshima City . . Hiroshima, Japan Daishowa Seishi Yoshmaga, Japan Daishowa Seishi . Suzukawa, Japan Sodersjukhuset Stockholm, Sweden No of units . . 1 1 2 1 1 1 1 1 1 1 5 1 3 Unit capacity (stdftVmm at 32° F) 50,000 75,000 159,000 17,700 10,000 31,300 83,000 66,400 48,300 10,000 44,200 14,700 17,700 Service Coal-fired boiler Oil-fired boiler Oil-fired boiler Black liquor boiler Secondary sludge incinerator Glass furnace Oil-fired boiler Oil-fired boiler Sintering plant Secondary sludge incinerator Oil-fired boiler Oil-fired boiler Oil-fired boiler Scrubbing reagent CaO and CaCOs dust NaOH NaOH CaO and CaCOs dust NaOH NaOH NaOH NaOH Ca(OH)2 waste carbide sludge NaOH NaOH NaOH Ca(OH)2 Table 9. R-C/Bahco Part:culate/S02 Removal Systems—Concluded Company and location Rickenbacker Air Force Base . . ... Columbus OH Kmo Ura Utility Japan Kanegafuchi Chemical . Takasago, Japan Grycksbo, Sweden Osaka City Osaka, Japan Central Glass Company Sakai, Japan Taio Paper Company lyomishima, Japan Yahagi Iron Works . . Nagoya, Japan Hiroshima City Hiroshima, Japan Daishowa Seishi .... .... ... Yoshmaga, Japan Daishowa Seishi .... Suzukawa, Japan Sodersjukhuset Stockholm, Sweden Inlet S02 concentration (ppm) .... . 400-2 000 1 500 1 400-1 530 4 000-6 000 70-80 1 200b 1 000- 1 500 1,000-1,500 2 500-4 000 900-1 000 900-1 200 800-1 500 S02 removal efficiency (percent) 70-90a 95-98 70a 50a 98 98 98 90-95 97 5 97-99 97-99 Date on line Mar 1976 Sept 1974 Apr 1973 Sept 1 972 Mar 1971 Mar 1971 Jan 1971 Jan 1971 Dec 1970 Dec 1970 Aug 3 1970 July 2, 1972 July 1970 Nov 1969 Apr 1970 Nov 1970 a Sufficient to meet local code b25 percent S03 ------- Environmental research and development of flue gas desulfurization programs is the responsibility of the Industrial Environmental Research Laboratory in Research Triangle Park NC. Mr. John Williams of the Emissions/Effluent Technology Branch is the Project Officer. Mr. Robert J. Ferb, of Research- Cottr.ell, is the principal contributor. EPA wishes to thank officials of the Rickenbacker Air Force Base, Columbus OH, for their cooperation and technical assistance. This report has been reviewed by the Industrial Environmental Research Laboratory, U.S. Environmental Protection Agency, Research Triangle Park NC, and approved for publication. Approval does not signify that the contents necessarily reflect the views and policies of the U.S. Environmental Protection Agency, nor does mention of trade names or commercial products constitute endorsement or recommendation for use. ------- |