United States
Environmental Protection
Agency
Municipal Environmental Research
Laboratory
Cincinnati OH 45268
EPA-600/2-80-016
June 1980
Research and Development
Evaluation of
Pollution Control
Processes

Upper Thompson
Sanitation District

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                RESEARCH REPORTING SERIES

Research reports of the Office of Research and Develbpment, U.S. Environmental
Protection Agency, have been grouped into nine series. These nine broad cate-
gories were established to facilitate further development and application of en-
vironmental technology. Elimination of traditional grouping was consciously
planned to foster technology transfer and a maximum interface in related fields.
The nine series are:

      1.  Environmental Health  Effects Research
      2.  Environmental Protection Technology
      3.  Ecological Research                  ;
      4.  Environmental Monitoring
      5.  Socioeconomic Environmental Studies
      6.  Scientific and Technical Assessment Reports (STAR)
      7,  interagency Energy-Environment Research and Development
      8.  "Special" Reports                    i
      9.  Miscellaneous Reports

This report has  been assigned  to the ENVIRONMENTAL PROTECTION TECH-
NOLOGY series. This series describes research performed to develop and dem-
onstrate instrumentation, equipment, and methodology to repair or prevent en-
vironmental degradation from point and non-point sources of pollution. This work
provides the new or improved technology required for the control and treatment
of pollution sources to meet environmental quality standards.
This document is available to the public through the National Technical Informa-
tion Service, Springfield, Virginia  22161.

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                                     EPA-600/2-80-016
                                     June  1980
 EVALUATION OF  POLLUTION CONTROL PROCESSES

    Upper  Thompson. Sanitation District
                    by
                Bob A.  Hegg
             Kerwin L.  Rakness
              Larry D.  DeMers
     M & I,  Inc.,  Consulting Engineers
       Fort  Collins, Colorado  80525
                    and
             Robert H.  Cheney
    Upper Thompson Sanitation District
        Estes Park, Colorado  80517
           Grant No. R-803831-01
              Project Officer
                Edwin Earth
       Wastewater Research Division
Municipal Environmental Research Laboratory
          Cincinnati, Ohio  45268
MUNICIPAL ENVIRONMENTAL RESEARCH LABORATORY
    OFFICE OF RESEARCH AND DEVELOPMENT
   U.S. ENVIRONMENTAL PROTECTION AGENCY
          CINCINNATI, OHIO  45268

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                                  DISCLAIMER
     This  report has been  reviewed by  the Municipal  Environmental Research
Laboratory, U.S.  Environmental Protection  Agency,  and approved  for publica-
tion.   Approval does not  signify that  the contents necessarily  reflect the
views and policies of the U.S.  Environmental Protection Agency, nor does men-
tion of trade names or commercial products constitute endorsement or recommen-
dation for use.
                                      ii

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                                   FOREWORD
     The  Environmental  Protection  Agency was  created because  of increasing
public and government concern about the dangers of pollution to the health and
welfare of  the  American people.  The  complexity of that  environment  and the
interplay between its components  require  a concentrated and integrated attack
on the problem.

     Research :and development is  that necessary first  step in problem solution
and it involves  defining  the problem, measuring  its  impact  and searching for
solutions.   The Municipal Environmental Research Laboratory  develops  new and
improved  technology  and systems  for the  prevention,  treatment  and management
of wastewater and solid and hazardous waste pollutant discharges  from munici-
pal and community sources,  for  the  preservation and treatment of public drink-
ing water supplies,  and to minimize the  adverse  economic,  social, health and
aesthetic effects of pollution.  This  publication  is one of  the  products  of
that research; a most vital communications  link between the researcher and the
user community.

     This  report describes  one of the  first municipal  wastewater treatment
facilities  specifically designed  for  two-stage nitrification and effluent dis-
infection with  ozone.
                                         Francis  T.  Mayo,  Director
                                         Municipal Environmental Research
                                         Laboratory
                                     iii

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                                    ABSTRACT
     The  Upper Thompson Sanitation District (UTSD) .advanced wastewater  treat-
ment  facility, located  in  Estes Park, Colorado,  incorporated several  unique
unit processes.   Among these were flow equalization,, attached  growth  nitrifi-
cation, mixed  media filtration and ozone disinfection.   Plant  design  flow  was
5,680 cu  m/day (1.5 mgd).   Average weekly  operating  flows  ranged  from  1,140 cu
ra/day to  3,790 cu m/day .(0.3 mgd to  1.0 mgd).  The  activated  sludge,  nitrifi-
cation and  filtration  processes  have  two parallel  trains.  By selectively using
one half  of the available units design flow conditions were achieved at one-
half  the plant  design flow  rate.   Therefore  the weekly average  flow  rates
during the  research project ranged from 40  percent  to  134 percent  of  design
and the BOD5 loading ranged from 14 to 228  percent of design.

     Overall plant  performance in terms of 6005  and TSS  removal was consis-
tent, averaging 95 percent  and  96 percent,  respectively.   Ammonia oxidation
was not as  consistent,  due  to loading extremes  and cold weather operating con-
ditions.  Performance  characteristics of  two nitrification  tower media  types
(plastic  dumped and redwood  slats)  were different.    The redwood  media per-
formed better  during cold weather  operation, but the recirculation (R/Q) ratio
was about 3 times higher than used for the  plastic  media.   The  plastic media
performed better during warm weather operation  (R/Q   ratios  similar).   Both
media types experienced periods  of solids  sloughing.  Neither media type per-
formed at a desired  optimum  performance  level although  design requirements
were achieved.

     The  mixed media filters  worked well for polishing  the nitrification tower
effluent  under  normal  conditions,  but  plugged  immediately   when  extensive
solids sloughing  from  the tower  occurred.   The  filters  were also used as part
of a  denitrification  study  to demonstrate  the effectiveness  of  dual purpose
nitrogen  removal  and  effluent polishing capability.  The  results showed that
denitrification  capability  existed when methanol  was added  to the filter  in-
fluent.    Filter plugging after relatively short filter  runs (2-3  hours) halted
the studies.

     The  air-fed  ozone  disinfection system was, operated intermittently because
of required modifications.   Special studies were  conducted  to determine per-
formance  information.    When operating,   good  disinfection   performance  was
achieved, but  high ambient  ozone  concentrations  in the  working environment
plus failure of materials exposed to ozone (piping and  diffusers) caused peri-
odic system shutdown.   Modifications  are indicated for  new ozone systems (not
completed at  the UTSD plant due  to  cost)  so  that more  cost  effective and
trouble free operating  systems might be possible.
                                     IV

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     The pressure filter sludge dewatering unit worked well in its application
at the UTSD plant, but  required  a relatively high polymer  usage  and cost due
to the type of sludge dewatered.

     This report  was  submitted in  fulfillment  of Grant  No.  R-803831  by the
UTSD  under  the  partial  sponsorship  of  the U.S.  Environmental  Protection
Agency.  This  report  covers a period from July  1975  to March 1979,  and was
completed as of May 1979.

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                                   CONTENTS
Disclaimer	«	    ii
Foreword ................ 	   iii
Abstract 	 ....... 	  ......  	    iv
Figures	°	•	viii
Tables	°	    ix
Acknowledgment	     x

     1.  Introduction  . . „	    -^
     2.  Purpose and Scope	    3
     3.  Conclusions	.	    4
     4.  Recommendations ............  	 ....   17
     5.  Description of Facilities 	  .......  	   19
         General	19
         Raw Sewage Pumping - Lift Stations  .......  	   21
         Flow Equalization .,	22
         Grit Removal	.  .	24
         Activated Sludge	25
              Aeration System	25
              Clarification System 	   26
              Sludge Pumping System	27
         Nitrification 	   28
         Mixed Media Filtration  	   30
         Ozone Disinfection	•	32
         Sludge Handling .	37
              Sludge Treatment	37
              Sludge Dewatering and Disposal 	   38
         Miscellaneous Facilities  	   41
              Stand-by Power	41
              Plant Laboratory	41
              Potable and Non-Potable Water Supply . 	   42
     6.  Data Collection and Analytical Procedures ...... 	   43
         Analytical Procedures and Quality Control 	 .....   43
         Analytical Schedule and Sample Type and Collection Frequency. .   46
     7.  Results and Discussion	50
         General	50
         Flow Equalization	51
         Grit Removal	55
         Activated Sludge  	   55
         Nitrification	65
              Plastic - Start-Up	70
              Plastic - Cold Weather	72
                                     vii

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                            CONTENTS  (Continued)
              Plastic - Warm Weather	  74
              Redwood - Start-Up  	 	 ......  78
              Redwood - Cold Weather	  79
              Redwood - Warm Weather	  82
              Redwood Update - Warm Weather	  86
              Redwood Update - Cold Weather  	 .....  87
              Overall Nitrification Evaluation 	 .....  90
         Denitrification	  91
              Start-Up Interval	» . . . .  92
              Methanol Full-Feed  Interval  .... 	 .....  95
              Filter Performance  (Physical Parameters) .........  99
         Mixed Media Filtration   	 .....  102
         Ozone Disinfection  	 .....  109
              General	  109
              Data Collection  	 .....  109
                   Ozone  in Air - Concentration and Mass Measurements  .  109
                   Ozone  in Water - Concentration Measurements .....  m
                   Electrical Power Consumption Measurements ......  112
                   Miscellaneous  Measurements  	 .....  112
              Data Evaluation and Discussion	113
                   Ozone  Air Pretreatment	  113
                   Ozone  Generator Production  .............  ng
                   Ozone  System Power Requirements 	  122
                   March  1979 Update	  130
                        Generator Flooding 	 .....  131
                        Dew Point Monitoring 	 .....  133
                        Generator Production Verses Dew Point  .....  133
                        Generator Power Requirements Verses Dew Point. .  134
                   Ozone  Contacting System 	 .....  134
                   Disinfection Performance  	 .....  141
         Sludge Dewatering and Disposal	  145
         Overall Treatment Plant  Performance 	 .....  151
         Operation and Capital Cost	  154
              Lift Stations  	 .....  154
              Flow Equalization and Grit Chamber 	 .....  155
              Activated Sludge 	 . 	 .....  155
              Nitrification  	 .....  156
              Filtration  	 .....  157
              Ozone Disinfection	,,....  153
              Sludge Handling  	 . . 	 .....  159
              Miscellaneous  	  160
              Summary of  Cost Information  	 .....  161
     8.  References	  163

Appendices	164
                                    viii

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                                   FIGURES
Number
                                                                        Page
   1    Plant flow schematic diagram of the Upper Thompson               •.•;...
        Sanitation District Wastewater Treatment Plant  ...;=.  .  .  .    20
   2    Equalization basin flow schematic diagram   .  .  i.  .;.  .  .  . .'•  .   • 22
   3    Ozone generation schematic diagram .  .  . .  ........  •  •    33
   4    Ozone contact basin schematic diagram  . .  ,; .  .  .  .  .  .  .  •  •   '35
   5    Mainstream sampling stations during the research  project  .  .  .    46
   6    Flow equalization basin influent and  effluent dissolved :.        -, :
        oxygen concentration	: •  •'-••  •    52
   7    Plant influent wastewater flow rate during  the  research
        project	  .•;-•>.«  .•••',  •    57
   8    Activated sludge influent BOD5 loading  and  effluent
        BODg residual	      57
   9    Activated sludge influent NIfy-N loading and effluent
        NIfy-N residual	      58
   10    Nitrification tower ammonia loading and ammonia oxidized
        during the research project   .	    69
   11    Nitrification tower ammonia loading and ammonia oxidized
        during the plastic start-up operating period 	 ...    70
   12    Nitrification tower ammonia loading and ammonia oxidized
        during the plastic cold weather operating  period 	    72
   13    Nitrification tower ammonia loading and ammonia oxidized
        during the plastic warm weather operating  period 	    75
   14    Nitrification tower ammonia loading and ammonia oxidized
        during the redwood start-up weather operating period  	    78
   15    Nitrification tower ammonia loading and ammonia oxidized
        during the redwood cold weather operating  period 	    80
   16    Nitrification tower ammonia loading and ammonia oxidized
        during the redwood warm weather operating  period .......    82
   17    Nitrification tower ammonia loading and ammonia oxidized
        during the redwood update warm weather and redwood update
        cold weather operating periods	    88
   18    Percent  N02/N03~N removal versus  methanol  to nitrate
        feed ratio for Period  A  and Period B  denitrification study .  .    97
   19    Filter head  loss  rate  during  Period A and  Period B methanol
        full-feed operating  interval  	    100
   20    Mixed media  filter  influent  and effluent  BOD5 concentration . .   106
   21    Mixed media  filter  influent and effluent TSS concentration .  .    106
   22    Comparison  of Dasibi meter and wet chemistry ozone/air
        concentration measurements	
                                      IX

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                              FIGURES (Continued)
Number                                                                  Page

  23    Change in air pretreatment dew point with drying tower
        operating time	117
  24    Change in ozone production with dew point at two generator
        power settings	  ..  118
  25    Ozone generator production at various generator power
        utilization	121
  26    Refrigerant drier operating time at various in-let air
        temperatures and an air flow rate of 79 cu m/hr (47 scfm) ...  124
  27    Measured power utilization for the existing UTSD ozone
        generation system 	  126
  28    Comparison of theoretical and actual UTSD ozone generation
        system power utilization  	 ....  129
  29    Schematic design of dew point cup and dew point measuring
        device	131
  30    Activated Sludge and overall plant ZOV$ removal efficiency
        during the entire research  project ... 	  153

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                                    TABLES
Number
   1    Fish Creek and Thompson River Lift Station Characteristics .  .   21
   2    Flow Equalization Basin Characteristics  	   23
   3    Grit Removal System Characteristics	   24
   4    Aeration Basin Characteristics 	   26
   5    Clarifier Characteristics  .... 	   27
   6    Activated Sludge Pumping Characteristics 	 .....   28
   7    Nitrification Tower Characteristics  	   28
   8    Mixed Media Filter Characteristics 	 . .  .   30
   9    Ozone Disinfection System Characteristics  	 	   32
  10    Aerobic Digester Characteristics 	   38
  11    Pressure Roller Filter and Sludge Hauling Truck
        Characteristics  	   39
  12    Description of Analytical Procedure Implemented During the
        UTSD Research Project	   44
  13    Analytical  Schedule for the Mainstream Samples  	   48
  14    Summary of Flow Equalization Basin Influent and Effluent
        Chemical and Microbiological Quality ...... 	   53
  15    Summary of Activated Sludge Performance for Operational
        Period I and Period IV	 . '	   59
  16    Summary of Activated Sludge Performance for Operational
        Period II and Period V ..............  	   62
  17    Summary of Activated Sludge Performance for Operational
        Period III and Period VI	   63
  18    Summary of Nitrification System Results  	   67
  19    Significant Events During the Plastic Start-Up Period  ....   71
  20    Significant Events During Plastic Cold Weather Period  ....   74
  21    Significant Events During Plastic Warm Weather Period  ....   77
  22    Significant Events During Redwood Cold Weather Period  ....   81
  23    Summary of Results During Redwood Warm Weather Period  ....   34
  24    Significant Events During Redwood Warm Weather Period  ....   85
  25    Significant Events During Redwood Update Cold Weather Period .   89
  26    Summary of Data Collected During Period A and Period B
        of the Denitrification Special Study .	   94
  27    Summary of Performance of Mixed Media Filtration System  . .  .   103
  28    Summary of Comparison of Continuous Measurement Dasibi
        Ozone Meter Results with Wet Chemistry Results 	   110
  29    Effect of Dew Point and Power Setting on Ozone Production  .  .   us
  30    Potential Decrease in Ozone Dosage for Observed Changes
        in Air Dew Point .	119
                                     xi

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                            TABLES  (Continued)
Number
  31    Summary of Power Consumption for the Air Pretreatment and
        Cooling Water Units  	  125
  32    Ozone Generator Power Requirements 	  127
  33    Total Ozone System Power Requirement at an Air Flow
        of 79 cu m/hr (47 scfm)	128
  34    Total Ozone System Power Requirement at an Air
        Flow of 118 cu m/hr (70 scfm)	128
  35    Comparative Dew Point Readings of Dew Point Cup
        versus Shaw Mini Hygrometer, March 15,1979	  132
  36    Summary of Ozone Disinfection Performance Data for
        Selected Time Periods	144
  37    Sludge Concentrator Performance During Start-Up 	  147
  38    Summary of Operation and Performance Data for 60-
        Day Period	  148
  39    Summary of Cost Data for Sludge Dewatering	150
  40    Summary of UTSD Plant Performance	152
  41    Capitol Cost—Upper Thompson Wastewater Treatment
        Plant	  161
  42    Annual Operating Costs - Upper Thompson Wastewater
        Treatment Plant	  162
                                    xii

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                               ACKNOWLEDGEMENT
     The  grantee  for  this project was the Upper Thompson Sanitation District.
Mr. Giles Gere, Chairman of the Board, was the Principal Investigator  for  the
research  effort.   M & I, Inc. served  as a  subcontractor for the District  and
acted as  the technical advisor  for  the research efort.


     Appreciation  is  expressed to all of  the  UTSD and M &  I,  Inc. personnel
who worked on the  research  effort.
          UTSD Staff:
               Plant Superintendent
               Lab Chemist
               Plant Operators
          M & I, Inc. Staff:

               Project Manager
               Project Engineer
               Project Technician
               Lab Chemist:
  Mr. Robert Cheney
  Ms. Barbara Baldwin
  Mr. Rawle Alloway
  Mr. Larry Boehme
  Mr. Roger Hess
  Mr. Tim Hunter
  Mr. Bob Tardy
- Mr. Bob Hegg
- Mr. Kerwin Rakness
-Mr. Larry DeMers
-Mr. Larry Stanton
— Mr. Jan Cranor
- Mrs. Sue Martin
     Appreciation is  also  expressed to Mr. Edwin  Barth,  Project Officer; Mr.

Al Venosa and Mr. Ed Opatken, EPA MERL - Cincinnati, Ohio, for their direction

and assistance regarding the research effort, and  to  Dr.  Sumner M. Morrison,

Colorado State University,  Fort Collins,  Colorado,  for technical  advice re-
garding microbiological testing.
                                     xiii

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                                  SECTION 1

                                 INTRODUCTION

     The Upper Thompson Sanitation District  (UTSD)  Wastewater Treatment Plant
is located near the mountain community of Estes Park, Colorado.  Estes Park is
the gateway city to the east entrance  of  the Rocky  Mountain National Park and
as such is highly tourist oriented.  The rivers in the area are scenic and are
used for many recreational purposes, including trout fishing.  In an effort to
protect the  uses  of the  Big  Thompson River  and  also to  protect  the tourist
industry of  the  area,  the  Upper Thompson Sanitation District was  formed to
provide wastewater treatment  services to the area  surrounding  the  Town of
Estes Park.   To  provide these services  a new wastewater  treatment  plant and
new collection sewers and interceptors were constructed.  The new plant incor-
porated:  flow equalization, activated sludge, fixed film nitrification, mixed
media filtration  and ozone disinfection.   The  inclusion of  this  variety of
processes  at one  plant  prompted the  United States  Environmental Protection
Agency (U.S.  EPA)  to fund a research  grant  to  evaluate the performance, cost
and design features of the  facility.   Data collection for  the research project
was conducted over a two  year period.   This  report  discusses the findings of
the research effort.
     The UTSD  plant  design flow rate was 5,680 cu  m/day (1.5 mgd).  However,
the  activated sludge,  nitrification and  filtration processes  were designed
with multiple  components,  and therefore, through separate use of  these  compo-
nents,  design loading  rates  could  be  achieved at  flow rates  less  than  the
total plant  design.   Initially, the wastewater flow rate from the newly  con-
structed UTSD  collection system was not expected to achieve  desired  flows  for
the  research effort, even if  only  half of the process  components were used.
Therefore,  as part  of  the  research  project, a  tie-line  between  the  UTSD

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 collection system and  the  collection  system from another District serving the
 Town of Estes Park was installed.  Supplemental flow from the Estes Park Sani-
 tation District  was  used  to  achieve  desired  flow  rates during  the research
 evaluation period.
      Two different types of media were evaluated for the fixed film nitrifica-
 tion process, namely  redwood  media and plastic  "dumped" media.   These media
 were evaluated during winter months to determine  the  effect  of temperature on
 the nitrification process.   Ozone was used at  the UTSD  for disinfection.   The
 ozone system  was  one of  the first  full-scale wastewater ozone  disinfection
 systems  in the United States.   Several "state of  the art"  problems were  en-
 countered and continuous operation was not achieved during the data collection
 phase of the  research project.   Some  system  modifictaions  were  necessary to
 achieve  continuous operation and others were  indicated to achieve  a more cost-
 effective operation.   The difficulties encountered during system operation  are
 presented in this report and  conclusions  are made concerning  various  aspects
 of  an ozone  system1s  operation,  maintenance and design.

      The  UTSD plant,  interceptor,  and collection systems were new and were
 started-up only  3 months before  the  research project was initiated.     Plant
 start-up  problems  were encountered  which were  compounded by a  major flood (Big
Thompson  Flood Disaster  -  July 1976  [1])  that washed-out a major  interceptor
line  that served  the  plant  (Thompson River Interceptor).   Considerable time
and effort were  expended to  recover from the effects  of the  flood and from a
variety of plant  start-up problems.  As an example,  lower than desired plant
flow  rates occurred  during the  first summer of  data  collection due  to a
reduced tourist trade in the community after the flood.

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                                  SECTION 2
                              PURPOSE AND SCOPE
     There were  several objectives  of the  UTSD research  project.    A major
objective was to evaluate  the  overall  performance,  cost and design aspects of
the UTSD  advanced  waste treatment  facility.  Additionally,  operating costs,
maintenance considerations  and costs,  and design  related considerations were
documented and evaluated for each unit process.  Evaluation of individual unit
processes  included  several special  aspects.   Two different  media  materials
were utilized in the  nitrification tower:   redwood  slat  and plastic  "dumped"
media.   Each media type was  operated for approximately  one  year  during the
data collection  phase of  the  research effort.   The project  also  involved a
special  study  to evaluate  denitrification  performance using  the  mixed media
filters (not an original design capability).  Methanol was added as the carbon
source  for  the  denitrification  process,  and  performance,   maintenance  and
design  aspects  regarding   denitrification  operation  using  the mixed  media
filters was evaluated.
     The  time  period  for the evaluation of  the  various processes ranged from
two  months  to two  years,  with  the  evaluation of  some processes overlapping
that of  others.   The wastewater flow that was treated was  all  the  flow from
the  UTSD collection system as normally  received,  plus some  of  the  flow from
the  Estes Park  Sanitation District  collection system.    The intent  was   to
achieve  a wastewater  flow rate  that  would allow most  of  the processes to  be
evaluated at design flow conditions  (i.e., accomplished by taking some of  the
multiple  components out  of service).

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                              SECTION 3
                             CONCLUSIONS
     The  flow  equalization basin  provided very  satisfactory  hydraulic
    dampening  of  the flow received  at  the  UTSD  wastewater  treatment
    facility.

    A.  Daily  average flows ranged from 15  percent  to 67 percent of  the
        5,680  cum/day (1.5 mgd)  plant design value, and no problems were
        encountered  with  sufficient  basin  storage  capacity  for  flow
        equalization.
    B.   The  basin effluent pinch valve flow controller assembly control-
        led  the flow rate +2% from the set rate, when functioning.

        1)   At very low  flow rates  the pinch  valve was  severely re-
             stricted  and maintenance  problems developed  with  the flow
             control assembly.

        2)   An isolation plug valve  located on the basin effluent line
            was used to  control  flow when the pinch valve was not work-
            ing, and the flow  rate  was controlled to a  variation  of +15
            percent of the set rate.

2.  Aeration and  mixing  were not provided in  the original design  of the
    UTSD flow equalization basin, but no major operational or performance
    problems were associated with this mode of operation.

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    A.   Fall, winter  and  spring basin effluent D.O.  concentrations  were
        above 1  mg/1.   Summer D.O. concentrations were below  1  mg/1,  but
        no odor  problems were evident.

    B.   Relatively low wastewater temperatures and/ or immediate  removal
        of settleable solids  from the  flow equalization basin  were  felt
        to be contributing factors  to  the absence of odor  problems  from
        the flow equalization system.

    C.   Other than D.O.  concentrations,  no significant  chemical  or  bio-
        logical  changes in wastewater characteristics occurred within the
        flow equalization basin.

    D.   A J.2 cm to 2.5 cm (1/2 in. to 1 in.) grease build-up occurred on
        the basin walls.   Periodic  cleaning prevented  further build-up
        and also prevented odor problems from developing.

3.  The aerated grit, removal  proces consistently performed  in a satis-
    factory manner.
4.   The  activated  sludge  process  experienced extreme  variations  in
    hydraulic and organic  loading,  and variable effluent  BOD5,  TSS,  and
       ~N concentrations occurred.
    A.  The wastewater  flow  rate and 6005 load  during  the project aver-
        aged less  than  design (i.e. design was  2840  cum/day (0.75 mgd))
        with one half  of the  activated sludge  units  in  service ,  but
        reached  a  level  much  greater  than  design during the  summer
        tourist  season.
        1)   Flow averaged 65  percent of  design,  but  reached  levels of
            134%  of design values.   The  6005 loading averaged  60 per-
            cent and reached levels of 228 percent of design values.

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    2)  High  flow and BOD5  loadings  during the  summer  tourist sea-
        son  of  the year  (3 months),  degraded activated  sludge ef-
        fluent quality.

B.  Low flow and  BOD5  loadings occurred during the  fall,  winter and
    spring seasons of the year (9-months), and nitrification occurred
    in the activated sludge process during a portion of that time.

    1)  During  this  period,  BOD5  loading  averaged 50  percent  of
        design.

    2)  Extensive ammonia  oxidation occurred  during the fall  until
        the Christmas  holiday tourist  season.

    3)  Ammonia  oxidation  abruptly stopped  when  the BOD5  load  in
        creased  by 140 percent during the  one-week Christmas  holiday
        season of  1976  and  1977.
   4)  Ammonia  oxidation did not re-occur after the Christmas  holi-
       day  flows subsided,  probably  due to the  low temperature  of
       the wastewater  (4-5°C).

   5)  Very low aeration basin biomass concentration was implemented
       during the fall of  1976 to discourage nitrification.  No con-
       trol over aeration  basin  dissolved oxygen concentration  was
       exercised.
       a)  MLVSS concentration was 920 mg/1.
       b)  Extensive nitrification was not eliminated.
       c)  BOD5 removal efficiency was 76 percent.

   6)  Higher aeration basin biomass concentration  was  implemented
       during the fall  of 1977  to  improve BOD5  removal.    No  con-
       trol  over aeration basin  dissolved oxygen  concentration   was
       exercised.

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            a)  MLVSS concentration was 2830 mg/1.
            b)  Extensive nitrification occurred.
            c)  BODg removal efficiency improved to 88%.

5.  The fixed-film nitrification process experienced extreme fluctuations
    in ammonia loading  and  wastewater temperature,  and variable ammonia
    oxidation occurred.  Each media type (redwood and plastic dumped) was
    operated under a start-up, cold weather and warm weather period.

    A.  For both media  types  the volume (one  side  of  tower) was identi-
        cal at  386  cu m (13S780 cu  ft).   Specific  surface  area for the
        plastic dumped  media  was 89 sq m/cu  m (27 sq  ft/cu ft) and for
        the redwood 46 sq m/cu m (14 sq ft/cu  ft).

    B.  Acclimation of  nitrifying  organisms  during  the start-up periods
        for both media  types  was severely limited because of low ammonia
        loading to the tower  (activated sludge system was nitrifying).

    C.  Cold  weather  operation for  both  media types  included  an abrupt
        increase  in  the ammonia  loading  to  the  tower following the
        Christmas holidays.   Different oxidation capabilities were  noted
        for  each media  type,  but different  operating  procedures   also
        occurred.
        1)   Overall oxidation performance  during  cold weather  operation
            for  both media  types averaged 25  percent for  the  redwood
            media  and 30  percent for  the  plastic media,  but good  pre-
            winter  start-up  conditions  did  not  exist.

        2)     Plastic   media   NH^N   oxidation   averaged  3.6   kg/day
            (8 Ib/day)  and  reached a  maximum  oxidation  of  6.8 kg/day
            (15  Ib/day).   The tower recirculation  ratio  (R/Q) was  rela-
            tively  low at  0.74.

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    3)  Redwood media NH^-N oxidation averaged 5.9 kg/day (13
        Ib/day) and reached a maximum oxidation of 9.5 kg/day (21
        Ib/day).  The tower R/Q ratio was 2.2.

D.  Warm weather operation for both media types included very high
    ammonia loadings (166 percent design), and different oxidation
    capabilities were noted for each media type.  Also, different
    operating characteristics were observed.

    1)  Plastic media oxidation capability initially increased rapid-
        ly during warm weather, and reached a maximum oxidation rate
        of 36 kg/day (80 Ib/day) or about 40 percent of the total
           ~N loading.  The R/Q ratio was 0.74.
    2)  Redwood media oxidation capability responded more slowly, and
        reached a maximum oxidation rate of 23 kg/day (50 Ib/day)
        which was also about 40 percent of the total NH^-N loading.
        The R/Q ratio was 0.77.

    3)  Both media types appear to achieve a maximum oxidation rate
        which would indicate that nitrification system design should
        be based on peak daily or peak weekly values.

    4)  Specific area (dry media) oxidation rates corresponding to
        the apparent maximum oxidation capability were:

           Plastic =1.03 gm/day/sq m (0.21 Ib/day/ 1000  ft2 media
           surface
           Redwood =1.27 gm/day/sq m (0.26 Ib/day/ 1000  ft2 media
           surface

        Plastic specific area oxidation rate was  20% less than red-
        wood,   but the plastic media had 52% more total  media surface
        area [i.e.   89 sq m/cu m (27 ft2/ft3) versus 46  sq m/cu m
        (14 ft2/ft3)].

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    5)  Excessive  solids  sloughing from the nitrification  tower im-
        mediately plugged the  mixed media filters and  occurred with
        both media types.

        a)    The  plastic  media   experienced  relatively  frequent
            (weekly) excessive solids sloughing conditions.

        b)  The redwood media experienced limited (monthly) excessive
            solids sloughing, and not to the extreme that was experi-
            enced with the plastic media.

E.   Important,  updated information concerning redwood  cold weather
    tower performance was  developed after the  data  collection  phase
    of  the  research project  was  over,  and  when  better  pre-cold
    weather tower start-up conditions were experienced.

    1)   Dissolved oxygen  control  in  the activated  sludge aeration
        basin was  used  to  inhibit  nitrification which allowed  higher
        ammonia loadings to the nitrification  tower.
    2)  An  average 94 percent  ammonia oxidation occurred in the fall
        of  1978  when   the  tower  loading was 26  gm/day/cu  m (1.6
        lb/day/1000  ft3) or 24 percent of design load.
    3)   Some increase  in ammonia  oxidation  occurred when the  1-week
        Christmas  holiday  ammonia load reached an  average 39  kg/day
        (85 Ib/day)  or 91 percent  of design.

        a)   Higher levels of  ammonia  oxidation were achieved  during
             this  higher  loading period, but  the  percent of incoming
            ammonia  oxidized decreased to a  low of 42 percent.
        b)   Acclimation of  the tower to  an expected higher  loading
            may be necessary through artificially feeding ammonia  by
            chemical  addition methods  prior  to  receipt  of  the  load.

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         4)   Subsequent  to the Christmas  holiday season and  during  cold
             weather  operation,   ammonia  load   dropped   to   pre-holiday
             levels.  Ammonia oxidation decreased from 13.6 kg/day  to  7.3
             kg/day (30 Ib/day to 16 Ib/day), while  tower  effluent  waste-
             water   temperature varied  from  1°C  to  4°C.    The tower  R/Q
             ratio  was  similar to  te previous winter  at  2.0, and the indi-
             cation was that  a significant  cold  weather  effect  on  nitrifi-
             cation performance occurred.

    F.   Bench  tests indicated that lower  temperature and  low  pH  signifi-
         cantly  reduced the  rate  of ammonia  oxidation,  but given  suffi-
         cient time complete  nitrification  always  occurred.

         1)   Lower  nitrification  rates are  probably experienced at  the
             UTSD Plant because of low winter time wastewater  temperature
             (1°C to 4°C) and  overall  lower  wastewater  pH and  alkalinity
             (typically less  than  6.5 and 100 mg/1, respectively).

         2)   Additional  time  (i.e. more  tower  media  by simultaneouly
             placing into  service both  towers)  and/or  higher  pH   (i.e.
             alkalinity addition)  may be necessary to consistently achieve
             high levels  of ammonia removal  under present loading  condi-
             tions  at the UTSD  facility.

     G.   Better  ammonia oxidation  capability  for  both media  types was
        associated  with  a higher R/Q  ratio   (i.e. greater  than 2  rather
        than less  than 1), although an optimum R/Q  ratio was  not  deter-
        mined.

6.   Denitrification capability was  the subject  of  a special  study and
    commenced when  methanol  was added  to the influent  to the  mixed media
    filters.  Extensive  filter plugging due  to biological growth  forced
    the study to be halted.
                                10

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    A.    An acclimation  time  of 7 days  was required  for  the  system to
        reach full NC^/NOg-N removal potentional.

        1)  Wastewater temperature was about 10°C..

     •   2)  Acclimation time excludes  the  time  when the amount of metha-
            nol added was  less than  the D.O.  requirement of  the waste-
            water.

    B.     To  achieve 90  percent  NC^/NOg-N  removal,  the  methanol  to
        nitrate (M/N) ratio was about 4.4.

    C.    Extensive filter  plugging  (i.e.  backwashing required  every 2-3
        hours)  occurred  within  2-3 weeks  and  caused the  study  to be
        halted.

7.  The mixed media  filter process worked well  to  polish  the nitrifica-
    tion tower effluent, but had  to  be bypassed when extensive sloughing
    of  solids from the tower occurred.

    A.   An  average 65 percent  to  75 percent reduction  in  the BOD^, TSS,
        and turbidity values occurred. Respective effluent concentrations
        were  10 mg/1, 6  mg/1 and 2.1  NTU,  excluding the  times  when the
        filter was  bypassed because  of plugging  problems due  to tower
        sloughing.

    B.   The tower's  excessive  solids  sloughing  caused the  filter to  plug
        within  10 minutes, and forced the filters  to  be  bypassed until
        sloughing ceased.
8.  The ozone  disinfection process was  the subject of  a special study.
    Several state of  the  art  problems occurred which hindered continuous
    operation, but  important  information was  developed  regarding system
    operation, maintenance and design as follows:

                                 11

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A.   The  "Dasibi Meter"  continuous measurement  ozone  concentration
    meter  readings  correlated well with wet chemistry results,  after
     the meter was  properly  set  up  and  calibrated.

    1)   Ozone  and purge  air flow to  the  meter was  controlled  at
        2  1/min.

    2)   The meter  span setting was adjusted  based on  wet-chemistry
        results.

B.  The ozone generator periodically "flooded" and was damaged  due  to
    malfunctions within the  air  pretreatment system.

    1)  A cobaltous chloride  color changing  indicator that was  pro-
        vided to show  an  increase  in air dew point was  not  sensitive
        to  gradual changes,  and potential problems  associated  with
        dew point could not  be detected  until far along.

    2)  A dew point meter was more sensitive to  gradual changes  in
        dew point,  but "flooding"   still occurred when the meter was
        monitored only once  per  day.

    3)  A dew point meter  with associated high dew point level  alarm
        and/or automatic  system shutdown would  substantially  reduce
        generator "flooding" potential.

    4)  The dew point meter  should  be checked against a  dew  point cup
        measuring instrument to verify meter accuracy and/or properly
        set the high dew point level alarm.

C.   The air  pretreatment refrigerant  drier  required  special   main-
    tenance considerations.
                             12'

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    1)  The drier voltage of  440 volts  was compatible with the volt-
        age of the ozone generator,  but required special order parts
        because 220 volt refrigeration  units  were more common in the
        community,)

    2)  Repairs to the refrigerant drier were quite technical and had
        to be completed by  an experienced repair man who had special
        equipment..

D. , More information should be developed by ozone equipment manufac-
    turers on ozone  production versus dew  point  levels over the en-
    tire ozone generator operation range, to provide design engineers
    and plant operators  with  a better  basis  for ozone system design
    and operation*

E.  Ozone  production  of  the  UTSD  ozone generators was  not signifi-
    cantly lower at air flow  rates of 79 cu m/hr  (47 scfm) as opposed
    to air flow rates of 118  cu m/hr (70 scfm).

F.  Ozone  generation  system power  utilization at  the  UTSD plant Was
    greater at  lower ozone production  levels due  to  the relatively
    constant  power  requirements of  the  air  pretreatment  unit,  and
    caused  inefficient  power  usage  under  current  operating  condi-
    tions.

    1)     Total   power   utilization   varied  from  about  55  kWh/kg
        (25 kWh/lb) at production levels of 0.32  kg/hr  (17 Ib/day) to
        33 kWh/kg  (15 kWh/lb)  at production levels  of  1.08  kg/hr
        (57 Ib/day).
    2)  Lower  ozone production levels of  0.32  kg/hr (17 Ib/day) are
        usually  sufficient  at the UTSD plant  for current wastewater
        flow rates  and  ozone  dosage requirements, thus the least ef-
        ficient  power utilization values presently exist.
                             13

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    3)  More efficient  power  utilization  values  over  the  entire  range
        of  ozone generation  system  operation would  improve system
        power  consumption and  cost  at lower  than design  wastewater
        flow rates  and  ozone  dosage requirements, and should be  con-
        sidered  for all ozone system  designs*

G.  Contact basin off-gas, ozone  discharge and other  sources  of  ozone
    leakage have caused excessively high  ambient  ozone concentrations
    in and around the plant  area, and, has required that  several  sys-
    tem design modifications  be made.

    1)  The contact basin had to  be totally covered and sealed.

    2)  The off-gas exhaust system was redesigned.

    3)  The basin baffles and scum skimmers were  modified.

    4)   The unplastized  polyvinyl  chloride (UPVC) ozone piping was
        replaced with stainless steel piping.

    5)  The ozone  off-gas must be destroyed.   A heat/catalyst ozone
        destruct unit was designed and constructed.

H.   An epoxy  joint on the  original ozone  diffusers was  not ozone
    resistant and failed.  As a result,  new diffusers with a mechan-
    ical joint had to be  installed.

I.  The UTSD ozone contact basin was designed  for 90 percent  transfer
    efficiency and was  based  on incomplete information.

    1)   Ozone  transfer  efficiency was  variable  and  was  affected by
        wastewater quality.
        a)  Typically,  the  transfer  efficiency was between 50 and 60
            percent.
                            14

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            b)   The  transfer efficiency  increased when  the wastewater
                quality was poor.

            c)  With good wastewater quality, measured ozone  transfer ef-
                ficiencies correlated well with ozone/liquid  gas transfer
                theory.

        2)  To  ensure achieving a desired,  minimum transfer efficiency,
            ozone contact  basin design  should  be  based  on  ozone/liquid
            gas transfer theory.

    J.  Good disinfection performance has occurred at the UTSD plant when
        the ozone  diffusers  were  in good condition and  the system was
        operated consecutively for several days.

        1)  Effluent fecal coliform concentrations averaged less than the
            design requirement of  200 per  100 ml  at applied ozone dosaes
            of about 7 mg/1.

        2)  When the ozone system was operated for only a short period of
            time, poor  disinfection  was experienced  and  increased ef-
            fluent TSS  concentrations occurred due to  biological  slime
            growth sloughing off of the contact basin walls and piping.

9.   The  sludge  dewatering unit functioned  very satisfactorily  in its
    application at the UTSD plant.

    A.   The sludge dewatered  during the research  period had  been con-
        tained in the aerobic digester for a long period of time, and was
        quite inert and difficult to dewater.

        1)  The VS/TS ratio was 58 percent.

        2)  The  specific  oxygen uptake  rate was  less than  0.5 mg/hr/gm
            VSS.
                                 15

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    B.    A  60-day  dewatering  test  was  conducted with the  following
        results:

        1)  The total amount of sludge dewatered during the 60-day period
            was 18.9 metric dry tons (20.8 dry tons).

        2)  The dry  weight percentage of  solids  in the dewatered sludge
            was 11 percent.

        3)   An average production  rate  of 99 kg/hr  (217 Ib/hr)  of dry
            solids occurred.

        4)  The polymer dosage required  was  25 kg/metric ton (50 Ib/ton)
            of dry sludge.
        5)  The polymer cost was ($62.22/ton) of dry sludge.

10.  The  total capital  cost for  the 5,680 cum/day  (1.5  mgd)  UTSD waste-
     water treatment  plant was approximately 3 million dollars.    The
     average operating cost at existing  wastewater  flow rates which were
     32 percent of  design  and  excluding  research-associated  costs, was
     $123,064 per year or 18.6<£/cum (70.3^/1000 gal) treated.
                                16

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                             SECTION 4
                          RECOMMENDATIONS
1.  Prior to  the peak  flow,  summer  tourist  season, acclimation  of the
    activated sludge  system for the  increased  loading should  be initi-
    ated.

2.  Modify operation  of nitrification tower  as  indicated by  results of
    the research project.

    A.  Place into service  both  sides of the tower to provide additional
        contact time  to  overcome the  nitrification rate reducing effects
        of the wastewater's low  temperature,  and relatively low alkalin-
        ity and pH values.

    B.   In  general,  maintain increased  tower  recirculation (R/Q) ratios
        and maintain  constant tower wetting rates.  Continue to evaluate
        performance to determine the  optimum R/Q ratio.

    C.   Discourage  ammonia oxidation  in  the  activated sludge system, by
        decreasing the D.O. concentration in the aeration basins.

3.  Substantially decreased filter hydraulic loading rates should be in-
    vestigated  with respect to  using mixed  media filters  for  the  dual
    purpose of denitrification and effluent polishing.

4.  Special considerations  should be  incorporated  into  ozone disinfection
    system designs.
                                  17

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A.  Incorporate a  dew point meter with a  high dew point level alarm
    and/or automatic  system shut-down  in  all  air pretreatment unit
    designs, in order to reduce generator  "flooding" potential.

B.  Require ozone generator manufacturers  to provide ozone production
    information for various dew point levels and for the entire ozone
    generator operating  range,  in order to  provide design engineers
    and plant operators  with a better  basis  for  ozone system design
    and operation.

C.   Provide  for  more  efficient  power  utilization over  the entire
    range  of  ozone  system production,  in  order  to  improve system
    power consumption and  operating  cost at lower than design waste-
    water flow rates and/or ozone dosage requirements.

D.  Base the design minimum transfer efficiences for ozone disinfect-
    ion system contact basins on ozone/liquid  gas  transfer theory,  in
    order to be assured of consistently good disinfection performance
    as well as consistently achieve expected ozone transfer efficien-
    cies.

E.  Provide  ozone destruction capability  for  the  contact basin off-
    gases.

F.  Provide suitable  grade stainless  steel piping for ozone gas dis-
    tribution.
                             18

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                                  SECTION 5
                          DESCRIPTION OF FACILITIES
     The Upper Thompson  Sanitation  District  (UTSD)  Wastewater Treatment Plant
was one of two plants serving the Town  of  Estes Park and the surrounding com-
munity.  The UTSD was  formed in 1971 to primarily  serve the area surrounding
the Town.  The Estes Park Sanitation District  served  the Town  of Estes Park.
The wastewater treated at both facilities was mostly domestic.

     The  UTSD  treatment  plant,  collection  lines,   and  a  portion  of  the
interceptor sewers were  constructed co-currently and were  placed in operation
in March,  1976.   Line  construction  in  the Estes Park area  was  expensive and
difficult  because  of the  rugged mountain terrain.    Delayed  construction  of
some of the UTSD collection  system  was  an  area of concern  with respect to the
volume of  flow that  would initially be  treated at  the UTSD  plant  during the
research project.   It  was  desired  to treat  a level of flow approaching the
design loading rate of the plant.  About 1,140 cu m/day (0.3 mgd) was expected
from the initial UTSD lines-  Additional flow was obtained from the Estes Park
Sanitation District  through a tie-line  that was constructed as part  of the
research project.

     Wastewater flow in  the  Estes Park  and UTSD service  areas varied signifi-
cantly from summer to winter because of a high  influx of  tourists  during the
summer months.    The  average  winter flow  at  the  UTSD  facility during  the
research project  was about 1,510 cu m/day (0.40 mgd), while the average summer
flow was about  3220 cu  m/day (0.85 mgd).   These averages included  the  flow
from  the  Estes  Park  tie-line.   The overall average plant  flow during  the
                                       19

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project was  1,930  cu  in/day (0.51 mgd),  and therefore about  70  percent of the
design loading was achieved by operating one-half of the plant units.

     A flow  schematic for  the UTSD facility  is  shown in Figure  1.  All waste-
water was pumped to the plant  from lift stations serving two river basins and
was directed to a  flow equalization basin.  Equalized flow was directed to the
grit  chamber  then to  the  activated  sludge  process.    Secondary clarifier
effluent was pumped over the nitrification  tower and was then directed to the
flow equalization  basin.   Equalized flow was directed to the grit chamber then
to the activated sludge process.  Secondary clarifier effluent was  pumped over
the nitrification  tower and was  then  directed to the mixed media pressure fil-
ters.  Filter  effluent was disinfected in  the  ozone  contact  basin, directed
through  a  filter  backwash  water storage   tank and  discharged  to  the  Big
Thompson River.   All  sludge produced in  the plant was  eventually settled in
the  secondary  clarifier.   Waste  sludge  and  scum was  pumped  to  an aerobic
digester for stabilization and  mass  reduction*   Digested sludge was dewatered
by a pressure  roller filter  and was  hauled  to  a sanitary  landfill.   All
FISH CREEK
Plant ^1
Influent 1
1
Plant j_
Influent


XTO Saniti
Landfill
Affluent To
Big Thompson
River
Wastewater Flow
Return Sludge
U/<*»tA eiurln*
LJU How Equalization 	
Station *"" f~fM\k
\ Aeration ^
. - - Grit
RIVER \ Chamber ,
Lift ^Rate Controller |?|
Station 	



1 1 Secondary
Aerobic T L Cfarifiers J
Sludqe ^ \ /
Concentrator j x. f
Digester | | 1 | 	 | T
iry '^' = ! ' * '
Nitrification ^E ' VJ(— — -^w
^. A Tower •*^*"^ zrz: waste Sludge j™
. . ..OyrtfV* ^nnta^t iww^i 	 «S^,,IYI ^



Tdiik i
Pressure Filters
	
         Figure 1.  Plant flow schematic diagram of the Upper Thompson
                    Sanitation District Wastewater Treatment Plant.
                                      20

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internal  side stream  flows were  directed back  to the  Thompson  River  Lift
Station.  A well equipped laboratory was provided for process evaluations.

Due to the elevation of the UTSD facility (2,290m (7,500 ft) above  sea level),
all treatment units except  the nitrification tower were covered for protection
from the weather as well  as for aesthetic purposes.   The nitrification tower
was open to the atmosphere  to allow for  oxygen  transfer.   About 0.91 m (3 ft)
of freeboard above the tower media provided for some weather protection.

RAW WASTEWATER PUMPING - LIFT STATIONS

     The UTSD collection  system served two drainage basins  in  the Estes Park
area, Fish Creek and Big  Thompson.  The  collection system in the Big Thompson
basin is the bigger of the  two,  and during the  research project about 90 per-
cent of  the total plant  flow was received  from this basin.   All wastewater
that was collected from both systems  was pumped to the  treatment  plant.   The
Thompson River lift station was located  at the plant site and  the Fish Creek
lift station about one-half mile from the plant.

     The lift stations consisted of a wet-well, dry-well,  pumps and a comminu-
tor  with bar screen  by-pass.   The  characteristics of  each lift  station is
shown in Table 1.
     TABLE 1.  FISH CREEK AND THOMPSON RIVER LIFT STATION CHARACTERISTICS
             Item
Description
  Fish Creek Lift Station
  Wet-Well Capacity
  Pumps
     Number
     Capacity (each)
  Communitor
     Number
     Capacity
 8,250 gal
 3 - 40 hp each
 900 gpm
    1
 4.0 mgd
                                                            (continued)
                                       21

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                             TABLE 1.  (Continued)
              Item
Description
  Thompson River Lift Station
  Wet-Well Capacity
  Pumps
     Number
     Capacity (each)
  Comminutor
     Number
     Capacity
 9,430 gal

 3 — 25 hp each
 1,350 gpm

     1
 7.4 mgd
gal x 3.785 =  1;  gpm x 0.0631 = I/sec; mgd x 3785 = cu m/day;  hp  x 0.746 = kw


FLOW EQUALIZATION


     Flow from both lift stations was directed to the flow  equalization basin.

Effluent flow  rates from the  basin were then controlled to provide a  consis-

tent flow rate to the downstream unit processes.  The flow  equalization system

was  constructed  to  dampen the  highly  variable daily  flow  rate  conditions

expected and to facilitate optimum  performance  of the downstream  processes  in

order to produce  a consistently high quality effluent.
1
TO
• CHAMBER
BASIN OVERFLOW
TO
GRIT CHAMBER
TO
KAMBER
t ,f

FLOW EQUALIZATION
BASIN WITH BOTTOM
SCRAPER
<\
\
ISOLATION VALVES^


y M r^ i_i r^
/ PINCH ^-MAGNETIC
/ VALVE FLOWMETER
^
INFLUENT VALVES
^
1
^DRAIN LINE
/ VALVE
k i
r
)
BYPASS VALVE—^j
'; — BYPASS VALVE
. 1
^THOMPSON LIFT ^
STATION INFLUENT
                                                          ,FISH CREEK
                                                           LIFT STATION
                                                           INFLUENT
                    EQUALIZATION BASIN
                    EFFLUENT
            Figure 2.  Equalization basin flow schematic diagram.
                                       22

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     The major components of  the flow equalization system include the equali-
zation basin, which was equipped with a  scraper' mechanism and  a water level
indicator-recorder;  a  magnetic  flow  meter with  inputs to a  flow indicator-
recorder-totalizer  and to  the  flow  control system;  and a  modulating pinch
valve complete with actuator  and automatic control  system.   A flow diagram
showing the piping location and  valves is  shown in Figure 2.   The basin char-
acteristics are shown  in Table 2.

              TABLE  2.  FLOW EQUALIZATION BASIN CHARACTERISTICS	
    Characteristic
           Description
Shape
Sidewater depth
Capacity of sloped area
Capacity of rectangular area
Total storage capacity
Scraper Mechanism - corner sweep
Rectangular with sloped bottom
12 ft
520 gal
324,900 gal
325,400 gal
0.5 hp
ft x 0.305 = m; gal x 3.785 = 1; hp x 0.746 = kW

     Equalized  flow was  obtained by means of  a pinch valve assembly,  located
on the  effluent line,  which was  operated and  controlled  by a combined  elec-
tronic/pneumatic  system  that  utilized  a flow signal  from a  magnetic  flow
meter.   Once a desired flow  rate was  obtained,  the pinch valve opened  and
closed as necessary to  compensate  for  an increase or decrease in  the  level of
the basin.   As  the level increased due  to a  higher basin influent flow  rate,
the pinch valve closed to compensate for  the  increased head which would  tend
to increase  flow above the desired rate.  Conversely,  as  the basin level  de-
creased  due  to a  lower basin influent  flow  rate, the  pinch valve opened  to
compensate for  the decreased head which would  tend to decrease flow below the
desired  rate.   The operation was  completely automatic,  and once a  flow rate is
set  it  is  maintained  unless  the basin  emptied.   The .set  flow  rate  could  be
exceeded if  the rate was  set to  low and  the basin filled and overflowed.

     No  aeration or mixing  of  the contents of  the basin was provided.   It was
expected that  septicity  conditions  in  the basin would not occur.   However,
                                      23

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provisions were made to add a  jet  aeration mixing  system  if  septicity  became a
problem.  Without  mixing,  settleable organic material which entered the  basin
was scraped to the hopper  discharge  and  immediately  removed.  As  such  the flow
equalization  basin did not provide  for  equalization of  the plant loading in
the form of settleable solids.

     The flow equalization system included the plant influent flow monitoring
system.  A magnetic flowmeter  was  used to provide flow information as well as
control of the pinch valve.   However, this meter  was bypassed  if the flow to
the equalization basin was bypassed to  the aerated  grit  chamber.  Under  this
condition plant flow could be measured  using  the  mixed media filter  effluent
flow measuring instruments.

GRIT REMOVAL

     The major components  of  the  grit chamber  include the grit basin, the air
diffusion system and the classification  equipment.   The grit system character-
istics are shown in Table  3.

                TABLE 3.   GRIT REMOVAL SYSTEM CHARACTERISTICS
   Characteristic
               Description
Shape
Volume
Settling Velocity
Grit Quality
Compressor
Rectangular with hoppered bottom
18,750 gal
1 ft/sec.
80 to 100 mesh
15 hp
gal x 3.785 - 1; ft/sec x 0.3048 = m/sec; hp x 0.746 = kW

     Flow from  the  equalization basin, flow bypassed  around the equalization
basin,  or  flow  that overflowed  the equalization  basin was  direcetd  to an
aerated grit chamber where grit material  was  settled out and collected in the
chamber's hoppered bottom.  The settled material was then pumped to a centri-
fugal classification unit where organic material that had settled in the cham-
ber was separated from the grit.   The dewatered grit material was then stored
                                      24

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in containers  for  disposal at a sanitary  landfill.   Air was  supplied to the
grit basin  to  provide a  method  of controlling  the  settling  velocity of the
material within the basin and to enhance grease flotation.  Grease retained in
the aerated grit chamber was manually removed.

ACTIVATED SLUDGE

     The major components of  the activated sludge process include the  aeration
system,  clarification system and  sludge pumping  systems.    A description of
each  system and a discussion of  the operational aspects  of  each  system is
presented below.

Aeration System

     The  aeration system was comprised  of  the  aeration  basins,  and  oxygen
transfer and basin mixing equipment.   Aeration basin mixing  and oxygen  trans-
fer was accomplished by  a  combination of mechanical  mixers (fixed pier  sub-
merged  turbine)  and  a supply of compressed  air.   Compressed  air from blowers
was  discharged into  the  aeration basins directly beneath the submerged  tur-
bines.   The compressed air formed large  bubbles  upon release  into  the  liquid
which were sheared  into  smaller  bubbles  and dispersed  by  the mixer.   The
required mixing  of the basin contents was supplied by  the  submerged turbines.

      Two identical  basins with  a common  center wall  were  provided.    Both
basins  were provided with separate influent flow control,  return sludge lines,
and air supply lines.   A dividing gate was  located  on the  common  wall sepa-
rating  the two  basins.   This gate  provided  for  flexible  use of the basins.
The basins  could be  operated independent  of one  another  or could be  used
together in a  variety of flow patterns.  During  the  research project the gate
was closed which allowed only one basin to be used.   The basin characteristics
are summarized in Table 4.
                                       25

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                    TABLE 4.   AERATION BASIN CHARACTERISTICS
    Characteristics
          Description
   Aeration Basins
   Number
   Surface Dimensions  (each)
   Sidewater Depth  (each)
   Capacity (each)
   Detention Time (No  recirculation
     included)
   One  Basin @  0.75 mgd
   Two  Basins @ 1.5 mgd
   Turbine Mixers
   Number (per  basin)
   Size
   Air  Blowers*
   Number
   Capacity (each)
   Size (each)
63 ft x 31 ft
17 ft
248,000 gal
7.9 hr
7.9 hr

2
25 hp
1200 scfm
75 hp
*Blowers also used for aerobic  digester air  supply.
ft x 0.305 « m; gal x 3.785 = 1; hp x 0.746  = kW; cfm x 0.028 = cu m/min


Clarification System


     The clarification  system  consisted  of  two clarifier basins  each with a
sludge collection mechanism.    The clarifiers were  center feed and peripheral

withdrawal units  and were  equipped with  both  a  surface and  bottom scraper
mechanism for  removing  scum and  sludge,  respectively.   Scum  was moved  to a

scum hopper and pumped to the  aerobic digester.  Sludge  was  returned back to
the aeration basin or was wasted.  Return sludge was withdrawn from the clari-

fier using a rapid withdrawal mechanism.  Sludge to be wasted was scraped to a
sludge hopper located at  the center of each clarifier and was pumped to the

aerobic digesters.   The  clarifier characteristics are summarized  in  Table 5.
                                     26

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                  TABLE 5.  CLARIFIER CHARACTERISTICS
   Characteristic
          Description
  Clarifiers
  Number
  Diameter (each)
  Surface area (each)
  Sidewater depth (each)
  Weir Length (each)
  Capacity (each)
  Overflow rate* 0.75 mgd
  Weir Overflow Rate*
  Hydraulic D.T.*
  Waste sludge hopper
  Location
  Capacity
  Sludge Mechanism
  Type

  Drive Motor
2
40 ft
1,256 sq ft
10 ft
126 ft      -
98,500 gal
600 gal/day/sq ft
5,970 gpd/ft
3.2 hr.

bottom of clarifeir
100 gal                   ,

Combined rapid withdrawal with
bottom scrapers
0,33 hp
ft x 0.305 = m; sq ft x 0.093 = sq m; gal x 3.785 = cu m gal/day/sq ft x 0.041
= cu m/day/sq m; hp x 0.746 = kW; gal/day/ft x 0.0124 - cu m/day/m
* One basin in service @ 0.75 mgd
Sludge Pumping Systems


     The activated sludge  pumping  system consisted of two return sludge pumps
and one  waste sludge pump.   The return  sludge  pumps were  variable non-clog
centrifugal pumps and could  be operated independently or  together.   The pump
discharge was  directed  to the  aeration basin, but  could be directed  to the
aerobic digester, if desired.   The  return sludge  flow rate was measured using
a venturi tube.   Flow rates were  indicated adjacent to the pumps  and  on the

main control panel.  The waste sludge pump was a  constant speed vortex pump.
The waste sludge flow rate was measured using a magnetic  type  flow meter and
was indicated  and  totalized.   A summary  of the characteristics  of  the acti-
vated sludge pumping system is shown in Table 6.
                                      27

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              TABLE 6.  ACTIVATED SLUDGE PUMPING CHARACTERISTICS
   Characteristics
           Description
  Return Sludge Pumps
  Number
  Type
  Capacity
  Return Sludge Flow Meter
  Number
  Type
  Waste Sludge Pump
  Number
  Type
  Capacity
  Waste Sludge Metering
  Number
  Type
2 - 5 hp each
Variable speed non-clog centrifugal
250 - 1200 gpm
Venturi Tube

1 - 1.5 hp
Constant Speed Vortex
100 gpm
Magnetic Meter
gpm x 0.0631 <- I/sec; hp x 0.746 = kW


NITRIFICATION


     Effluent from the activated  sludge  system was  directed to a wet-well and

pumped to an attached growth nitrification  tower.   The tower media was origi-

nally designed to be redwood slats.  However, in conjunction with the research

project the tower was divided  into two equal sections and  two types of media

(redwood and dumped  plastic)  were installed.   Flow could be  directed  to one

side of the tower only, or to both sides depending on flow conditions.  During

the research project only one side  of the  tower was  operated at a  time.   A

summary of the nitrification system characteristics is shown in Table 7.
                TABLE 7.  NITRIFICATION TOWER CHARACTERISTICS
   Characteristic
           Description
  Wet-Well Capacity
  By-Pass
  Pumps
  Number
    59,500 gal
    Overflow to ozone contact basin

    2 - 30 hp each
                                                         (continued)
                                      28

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                            TABLE 7.  (Continued)
   Characteristic
       Description
  Type

  Capacity (each)
  Nitrification Tower
  Media Depth
  Surface Area (one side)
  Volume (one side)
  Hydraulic loading rate (each side)
    @ 0.75 mgd and no recycle
  Ammonia loading rate (each side)
    @ 0.75 mgd and 15 mg/1 NH4~N
  Recycle Rate (maximum)
    @ 0.75 mgd and one pump
  Media (Specific Surface Area)
  Redwood Media
  Plastic Dumped Media
  Distribution System
  Type
  Nozzles
Variable speed non-clog
centrifugal pumps
0 - 2250 gpm

14 ft
984 sq ft
13,780 cu ft

0.53 gpm/sq ft
6.8 Ib NH/t-N/day/1000 ft3
4:1

14 sq ft/cu ft
27 sq ft/cu ft

Fixed
Vari-flow
ft x 0.305 = m; sq ft x 0.093 = sq m; cu ft x 0.028 = cu m; sq ft/cu ft x 3.28
= sq m/cu m; gal x 3.785 = 1; gpm x 0.0631 = I/sec; gpm/sq ft x 40.7 =
1/min/sq m; lb/day/1000 ft3 x 16 = sq m/cu m; hp x 0.746 = kW.


     Two variable speed non—clog centrifugal pumps were used to pump activated

sludge effluent  to  the nitrification  tower.   Secondary  effluent  was distri-

buted over the tower surface through a fixed nozzle distribution system.  The

nozzles that  were originally installed  had a fixed  splash plate  design and

poor flow  distribution over  the  media  surface  occurred especially  at  lower
flow conditions.  These  splash plates  were later  replaced  with spring loaded

splash plates  (Neptune Microfloc Vari-flow  nozzles) and good distribution was

obtained even with variable flow rates to the tower.


     Flow  through • the  tower was directed  to a  wet-well located  beneath the

tower.   Gravity flow from the wet well was directed to the mixed media filters

(the level of  flow in  the  wet  well served to pressurize  the  filters).   Addi-

tionally,   a  controlled  and  measured   portion  of  the  tower   flow could  be
recycled back to the towers.
                                      29

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MIXED MEDIA FILTRATION


     The filtration system consisted of a chemical addition and rapid mixing
system, four pressure filter vessels, a backwash water storage basin and a

backwash wastewater storage basin.  A summary of the mixed media filtration

system characteristics is shown in Table 8.
                 TABLE 8.  MIXED MEDIA FILTER CHARACTERISTICS
   Characteristic
         Description
  Mixed Media Filters
  Number
  Shape

  Media Surface Area (each)
  Media
  Underdrains

  Surface Wash (each)

  Vessel Relief Valves
  Loading Rate
    Recommended
    Actual @ .75 mgd with 2 filters
  Backwash System
  Backwash Pumps
    Number
    Type
    Capacity (each)
    Backwash Supply Storage Volume
  Surface Wash Pump
  Number
  Type
  Capacity
  Backwash Wastewater Basin
  Storage Volume
  Discharge
  Chemical Feed Systems
  Feed Pumps (Alum)
      Number
      Type
      Capacity
    Alum Storage Volume
Cylinderical (8 ft diameter x
  18 ft long)
144 sq ft (8 ft dia x 18 ft long)
Anthracite coal, sand and gravel
Perforated PVC pipe lateral
  placed in support gravel
Three - six foot diameter water-
  jet rotary sweep.
Air and pressure relief valves

5 gpra/sq ft
3.. 6 gpm/sq ft
2 - 40 hp each
Constant speed centrifugal
2,500 gpm
42,000 gal

1 - 15 hp
Constant speed centrigual
200 gpm

40,000 gal
Thompson River Lift Station
Diaphragm
2 to 50 gph
4,000 gal
                                                           (Continued)
                                      30

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                          TABLE  8.   (Continued)
   Characteristic
         Description
    Polymer Feed Pumps
      Number
      Type
      Capacity
    Polymer Preparation
    In-Line Mixer
Diaphragm
1-22 gph
Dry Polymer Mix System
1 - Walker Process Instro-Mix
sq ft x 0.093 = sq m; ft x 0.305 = mj gpm/sq  ft x 40.7 = 1/min/sq m;
gpm x 5.45 = cu m/day; gal x 3.785 = 1; gph x 0.091 = cu m/day; hp x 0.746=kW.'

     A coagulant aid could be  added  to  the influent to the filters through  an
in-line flash mixer.  Liquid chemical  storage and feed pumps and dry  chemical
preparation and feed pumps were  provided  as  part  of the coagulant aid  system.
Chemicals could  also be added at  the  effluent weir  of  the  activated  sludge
aeration basins  and at the  nitrification tower  wet  well.   This flexibility
allowed the  chemical feed system to be used to add  chemicals  for phosphorus
removal and/or chemicals  for  alkalinity adjustment.  As  part of the  research
project a methanol  feed  system was installed whereby methanol  could be added
to the mixed media  filter  influent  at  the in-line mixer.   The  purpose of the
methanol addition was  to  evaluate denitrification  capability using  the media
of the filters to support the  denitrifying organisms.

     The filter backwash sjrstem was  provided  to release and return all  parti-
cles that had been  trapped  in  the  filter media to the head of  the  plant.    An
automatic system  for  initiating and  controlling  the  backwash  sequence  was
provided.  When the head loss  through  a filter reached a predetermined  level,
the filter was ,taken off line, backwashed  and returned  to service.   The back-
wash cycle could  also  be  initiated manually  by the plant  operators  and this
procedure was  used during  the pro'ject.   Components  of  the  backwash  system
included the backwash  water storage basin,  backwash and  surface  wash  pumps,
and the instrumentation and control equipment to operate the  system.
     The backwash water  storage  basin was  located directly beneath the admin-
istrative  offices,  and  contained  ozonated plant  effluent.   A  morning glory
                                      31

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overflow weir in the basin directed plant effluent from  the basin  to  the plant
outfall line.

     Backwash wastewater from  the  filters was  stored in a  concrete storage
basin  located beneath the  laboratory.    The discharge from  the  basin  was
directed   to  the Thompson River Lift Station at  a  controlled rate, pumped to
the flow equalization  basin  and directed back through  the plant.

OZONE DISINFECTION

     The UTSD ozone disinfection process was one  of the  first full-scale ozone
wastewater disinfection processes in the United States.  Several "state of the
art" problems were encountered  and  modifications to the original  ozone system
design were necessary.  In this section of the report  the ozone system is des-
cribed as it was modified.   The reason for and the extent of  the modifications
are discussed later in the report.   Ozone  disinfection was  an area of special
study; consequently, the  following  section contains a detailed description of
the disinfection system.

     The ozone disinfection  process consisted of two  air-fed ozone generator
units and  one ozone  contact  basin.   Each generator unit was  designed to pro-
vide adequate disinfection at the plant  design  flow rate.   The second genera-
tor  unit  was provided for  stand-by.    The  two  units were  identically  con-
structed and  were  labeled No.  1  and No.  2.   A  summary of  the  ozone system
characteristics is presented in Table 9.
             TABLE 9.  OZONE DISINFECTION SYSTEM CHARACTERISTICS
   Characteristic
          Description
  Generation System
    Number
    Air Pretreatment (2 units)
      Components
      Capacity
Compresser(15 hp each), cooler,
drying tower
78 scfm (drying tower limitation)
            (Continued)
                                      32

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                            TABLE 9.  (Continued)
   Characteristic
                  Description
      Dew Point (maximum)
    Generator (2 units)
      Manufacturer
      Type
      Capacity @ 1% by weight
      Dosage @ 1.5 mgd
    Cooling System (1 unit)
      Media
      Capacity
  Contact Basin
      Ozone Transfer
    Shape

    Volume
    Detention Time @ 1.5 mgd
        -51°C

        We Isbach
        "Iron Lung"
        76 Ib/day
        6 mg/1

        Well Water
        20 gpm

        Fine Bubble Tube Diffusers
        Rectangular, with vertical ser-
          pentine flow pattern
        14,500 gal
        14 min
cfm x 0.028 = cu m/min;  Ib/day x 0.454 = kg/day;  gpm x 0.063  = I/sec;  gal  x
3.785 = 1; mgd x 3785 = cu m/day; hp x 0.746 = kW.


     Ozone was generated by  two  Welsbach air-fed units,  Model CLP-68F20L.  A
schematic diagram  of the  ozone  generation equipment  is  shown  in  Figure 3.
     AIR
                 BLEED OFF
           COMPRESSOR    1
TO AIR	
PRETREATMENT
r N

;
\ 	 /



^_


REFRIGERANT
DRYER
"SEPARATOR
— 	 ^

                                                     I
                                                    1
      POWER

WATT-HOUR
METER
                      •TO CONTACT
                       BASIN

LEFT











RIGHT



CONTROLLER—"
c

GENERATOR 	 *
E
	 ^ 	
-y


^^^^^
             DRYING   TOWERS
               Figure 3.   Ozone generation schematic  diagram.

                                     33

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Three  components  made up each  system:   generator, power  supply  and air pre-
                                                           ^
treatment.  Each  generator  was designed to produce  1.43  kg/hr (76 Ib/day) of
ozone  at a minimum  concentration  of  1  percent by weight,  which provided for a
maximum  ozone/liquid dosage of 6 mg/1 at  the  plant design flow  of 5,680 cu
m/day  (1.5 mgd).   The generators were "iron lung" tube  type  units each con-
taining 68 tubes.   The generators were water  cooled  using potable well water
flowing at a rate of  approximately 1.26 I/sec (20  gpm).   Power was  supplied to
the generator  through variable voltage  transformers.  A controller assembly
was used  to  adjust the voltage from the transformer  to  the generator, which
controls the ozone  generator output.  The  controller was designed for manual
or automatic adjustment.  During  the research project manual adjustments based
on generator amperage readings were used.

     The air  pretreatment components  of  the ozone generation  system were an
air compressor, refrigerant  drier and  air drying towers.   Air pretreatment was
designed to provide particle-free dry  air with a dew  point of -51°C at  a pres-
sure between  41.3 k  N/sq m and  103   k N/sq  m  (6 and  15 psig).   During the
research  project,  the air  pretreatment  pressure was maintained at  51.6 k
N/sq m (7.5 psig).

     Ambient air was  compressed to 51.6 k N/sq m (7.5 psig) by a Nash Model L3
water ring compressor.  The  compressor operates at a  constant speed and had an
output of about 160 cu m/hr  (94 scfm).  The standard conditions used through-
out this report  are one  atmosphere  pressure  and  25°C  temperature.   A baffle
separator was  provided to separate the water and  air.  A bleed-off air valve
was provided downstream of  the  baffle  separator.   The bleed-off valve at this
point was determined  to be necessary during the research  project to enable the
air flow rate  to  the  drying  towers  to  be  controlled  to prevent overloading of
these units.
     Compressed air was cooled  to  between  3.3°C  and 5.6°C in a Zeks, Model 9J
refrigerant drier,  in order to remove  excess  moisture in the air.   The unit
was designed so that  the air dew point  leaving this unit  did not exceed 8.9°C.
Refrigerant dried air was further  dewatered  to a dew point less than -51°C in

                                      34

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a Kemp Model 100 UEA-1 absorptive drier.  The drier  used  molecular  sieves  and
activated alumina as absorptive material.  Dual  towers were  provided  for  con-
tinuous operation.  Tower operation was  cycled at  8-hour  intervals  to provide
regeneration of one tower while the other was in use.  Each tower was  rated by
the manufacturer at 131 cu m/hr (78 scfm) air flow.

     The ozone contact basin was  located adjacent to the mixed  media filters
in the main  control building.   The ozone generation units  were located on  a
mezzanine above the contact basin.  The  ozone  contact basin was  1.30 m  (4.25
ft) wide, 11.6 m  (38.0 ft) long and  3.66 m  (12  ft) deep, which  would give an
ozone contact  time  of  14 min at  5,680  cu m/day (1.5 mgd)  design flow.   The
first 8.22 m (27 ft) of the ozone basin was  divided into  nine equal  sized  com-
partments with U.P.V.C. baffles.   The baffles  were  placed to  allow vertical,
serpentine flow  of  effluent  through  the basin.   A  schematic  of the  contact
basin is shown in Figure 4.
                          BACKWASH
                          EiASIN
OVERFLOW
WEIR^
      " COVER
       PLATES)
         -Q
             DRAIN
                  6666
                                                        OZONE
                                                        DESTRUCT UNIT
                                                        CONTACT  BASIN
                                                        VENT
                                                        INFLUENT
                                                        UPVC  BAFFLE
                                                        OZONE  DIFFUSER
              Figure 4.  Ozone contact basin schematic diagram.
                                      35

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     Treated water from the ozone basin passed  over  a weir and into the back-
wash water  storage basin  where it  is  used for  backwashing the  mixed media
filters.  The ozone contact basin and the backwash water storage basin share a
common air  space  above their respective  water  surfaces due  to  the described
overflow weir arrangement.

     The contact basin was covered  with aluminum plates which were bolted in
place.   Hypalon gasket material was  placed  beneath  all joints.  Additionally,
silicone sealant was  used to cover  all exposed joints.   Ozone  laden off-gas
from both the contact and backwash water storage basins was discharged through
a rpof mounted exhaust fan.   The  fan provided  a negative pressure (about 0.64
cm of water) in each  basin so as  to prevent ozone leakage  into  the main con-
trol building and/or  offices.  A water spray  nozzle was located  in the vent
duct above  the ozone basin  tank cover  to prevent  foam  from  blocking  the
exhaust air flow.

     Ozone was injected into  the  effluent in the contact basin through porous
stone diffusers.   The  diffusers  were Kullendite,  Model  FAO 50  as manufac-
tured by Ferro  Corporation.   The diffusers  were located in each  of the nine
baffled areas.  Each diffuser was 6.4 cm  (2-1/2 in)  in diameter and 61 cm (24
in) long, and had  an  air  permeability between  1.42  and  1.78  cu m/min/sq m/cm
(12 and 15  scfm/ft^/in) and  a maximum pore  diameter  of  140 microns.  Distri-
bution piping consisted  of Type 304 Schedule  40 stainless  steel piping with
welded and  threaded joints.   Distribution  of  ozone to each  compartment  was
controlled  by  nine individual  valves.    Both  the diffusers  and distribution
piping represented modifications of  the original equipment.

     Four adjustable  height  weir  scum skimmers  were located along the length
of  the  ozone contact  basin  to facilitate  removal  of any  scum that  may be
generated as a  byproduct of  ozonation.   Scum  removed by the  skimmers can be
pumped to the head of the  plant for  recycle, or pumped to the secondary clari-
fiers.
                                      36

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     An ozone  off-gas destruct unit  is shown in  Figure 4.   The  unit  was a
heat/catalyst ozone destruct system which was installed after the data collec-
tion phase of the project was  completed.   The ozone destruct unit  represented
a major  design  modification,  which  will  be  further discussed.    The  ozone
destruct system was designed  by Emery  Industries  and  consisted of an off-gas
heating unit, a  proprietary catalyst,  and  an exhaust  fan.   The system design
inlet flow rate was 5.6 cu m/min (200 scfm) and the inlet temperature was 5°C.
The heating system was capable  of  elevating  the  temperature of this volume of
the off-gas to a maximum value  of  149°C (300°F).   At this maximum  temperature
the heat-catalyst system was designed to discharge a very low maximum residual
ozone concentration of 0.1  ppm (vol) when the heat/catalyst inlet ozone con-
centration was  3,000 ppm  (wt) or  lower.   At  this heating  requirement,   the
system was designed with a variable heating system and normal system operation
called for an operating temperature  of  71°C  (160°F).   At this temperature  the
system, was  designed to discharge  a maximum residual  ozone concentration of
1.0 ppm (vol) when the inlet  ozone  concentration  was  3,000 ppm (wt) or lower.
At  this  normal operation heating  requirement,  the power  consumption  for  the
system would be 7.5 kW for heating plus 0.5 kW for the exhaust fan.

SLUDGE   HANDLING
                                     t

     The sludge  handling system consisted  of  two  aerobic digesters, one pres-
sure roller filter, and one  sludge hauling vehicle.   The digesters were used
for  sludge  holding,   digestion  and partial  thickening.   The  pressure roller
filter was used for further sludge dewatering prior to ultimate disposal.   The
sludge hauling truck  was used to transport the thickened sludge to the ulti-
mate disposal site.

Sludge Treatment
     Sludge  treatment  was provided  by aerobic digesters,  which included  the
digester  basins,  oxygen  transfer  and basin  mixing,  supernatant  removal  and
sludge  removal systems.   A  summary  of  the  characteristics  of  the aerobic
digestion system is presented in Table 10.
                                      37

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                 TABLE  10.  AEROBIC DIGESTER CHARACTERISTICS
             Characteristic
  Description
      Aerobic Digester  Basins
        Number
        Surface Dimensions  (each)
        Sidewater Depth (each)
        Capacity (each)
      Turbine Mixers
        Number (per basin)
        Size
      Air Blowers*
        Number
        Capacity (each)
        Size
63 ft x 31 ft
17 ft
246,000 gal

2
25 hp
1200 scfm
75 hp
    ft x 0.035 « m; gal x 3.785 =1; hp x 0.746 = kW; cfm x 0.028 = cu m/min
   *Blowers also used for aeration basin oxygen supply.


     The aerobic  digesters  received waste sludge and  scum  from the secondary

clarifiers.   Two  digester  basins  were provided,  and  could  be  operated in

series or in parallel.  Oxygen supply and basin mixing were provided by a  sub-

merged turbine aeration system, which were identical to  the system provided in
the activated sludge aeration basins.


     Each basin  had supernatant  and  sludge  removal capability.   Supernatant

removal was used  to  partially  thicken the digested sludge  and to improve the

performance of the digestion process and the sludge dewatering pressure roller

filter.   Supernatant flow  was directed  to  the  Thompson  River  Lift  Station

where it was pumped  to  the  flow  equalization basin and  recycled back through

the plant.   The  sludge removal piping  was  located  beneath the   floor  of the
basins and was used to transport  sludge to  the  pressure  roller filter.   These

lines could  also be used  to drain  the basin  contents  back  to  the  Thompson

River Lift Station.


Sludge Dewatering and Disposal
     Digested sludge was dewatered prior to ultimate disposal with a Smith and
Loveless Model 40-1 pressure roller filter.  The pressure roller filter system

                                      38

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consisted of a  sludge conditioning unit  (sludge  feed pump,  polymer  mix tank

and metering pump, flash mixer  and  flocculator), • and a sludge dewatering unit

(primary and secondary screens, spray  cleaning  jets, transition  chutes,  and

three double  pressure rollers),  and  a  sludge transportation  unit (conveyer

belt from dewatering  unit  to sludge  hauling vehicle).   Dewatered sludge was

hauled to the disposal site with a covered  dump  truck,  which  had a modified

dump body so that it was watertight.  A summary  of the characteristics of the
pressure roller filter and sludge hauling truck is given in Table  11.

  TABLE 11.   PRESSURE ROLLER FILTER AND SLUDGE HAULING TRUCK CHARACTERISTICS
   Characteristic
                    Description
  Sludge Conditioning Equipment
    Sludge Feed Pump
      Type
      Capacity
    Polymer Mix Tank
      Type
      Volume
    Polymer Feed Pump
      Type
      Capacity
    Flash Mix
      Tank Size
      Mixer Drive
    Flocculator
      Tank Size
      Flow Pattern
      Paddle Drive
  Sludge Dewatering
    Primary Stage
      Screen Type
      Screen Size
    Secondary Stage
      Screen Type
      Screen Size
    Pressure Rollers

    Transportation Stage
      Conveyer Belt Size
  Sludge Hauling
    Vehicle Type
    Capacity
         Variable speed, diaphragm pump
         0 - 40 gpm

         Fiberglass
         250 gal

         Variable speed gear pump
         0-1.5 gpm

         12 in Dia. x 42 in long (21 gal)
         0.5 hp (variable speed)

         48 in x 24 in x 46 in (230 gal)
         Horizontal Serpentine Flow
         0.5 hp (variable speed)
         Endless, mono—filament open mesh
         40 in wide x 46 in long

         Endless, mono—filament open mesh
         40 in wide x 48 in long
         3 sets with variable pressure
           adjustment

         16 in wide' x 24 ft long

         Covered watertight dump truck
         7 cu yd
gpm x 0.063 = I/sec; gal x 3.785
0.305 = m; cu yd x 0.765 = cu m.
1; in x 2.54 = cm; hp x 0.746 = kW; ft x
                                     39

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     Sludge from  the digester was pumped  at  a controlled  rate  to the  sludge
conditioning system.   Polymer addition involved  the  injection of a stream  of
polymer solution into  the sludge feed line.  The  mixture of  polymer and  sludge
then entered a flash mixer where rapid mixing  dispersed the  polymer throughout
the sludge particles.  A flocculator followed  the flash mixer, and the mechan-
ism provided a plug flow condition together with  gentle agitation.  The  condi-
tioned sludge then entered  the primary stage of  the sludge  dewatering segment
of the system.

     The primary  stage of  the dewatering  unit consisted  of an endless, hori-
zontal, open-mesh  screen  which traveled around two rollers.   A  third  roller
was located midway between the two end rollers and resulted  in a  slightly  ele-
vated portion of the screen.  As the conditioned  sludge moved  onto the primary
screen, the free water drained away  and the flocculated sludge particles  were
trapped on the screen.  Further release of water was  obtained by passing  the
sludge over the elevated  roller.   At the  end  of  the  primary stage the  sludge
was transferred to  the secondary stage  of the dewatering unit.   A jet spray
bar  located  above  the  returning  portion  of  the   primary  screen  cleaned
entrapped sludge  particles  from the  screen mesh.   The filtrate  from the  pri-
mary stage,  which consisted  of  the  released  water,  non-captured sludge,  and
spray water, collected in a drain located  below the primary  screen.

     Sludge  from  the  primary stage  was  transferred  to  the  secondary stage
where it was deposited onto a screen identical to the primary screen.  Three
sets of  pressure  rollers were located along  the  secondary screen,  each  set
having one roller above and one  roller below the upper portion of the screen.
As the sludge moved  from one  set  of  rollers to the next,  progressively  higher
pressure was applied to the  sludge.   With this arrangement  water  was  squeezed
from the sludge three  times before leaving the dewatering  unit.   The resulting
sludge cake dropped  to a conveyor  system where it was transported to a  truck.
Similar to  the primary screen,  the  secondary screen  had a jet  spray bar  to
clean, the sludge  particles  trapped in the  screen mesh.   Released water,  non-
captured sludge, and spray water  from the secondary stage were collected  in a
                                      40

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drain and together with the primary  filtrate  flowed back  to  the Thompson River
Lift Station then back through  the plant.

     The  conveyer system that  transported  dewatered sludge  to  the sludge
hauling truck was equipped with a scraper  that  cleaned the conveyer  belt prior
to its return cycle.   The sludge hauling  truck was a covered dump  truck  that
was modified  so  that the tailgate was  watertight.   Also,  special  gate latch
hooks were provided  to prevent  the  gate from accidently opening during trans-
port to the disposl  site.  Two sludge  disposal  sites were utilized,  the  com-
munity sanitary  landfill  and community park  areas that were being  reclaimed.

MISCELLANEOUS FACILITIES

Stand-by Power

     The plant and lift stations  were provided three different power  sources:
Big Thompson loop power and South loop  via the Estes  Park substation, and  two
stand-by generators (one  at the plant and  one at  the  Fish Creek Lift Station).
The power supply automatically switched to the other power  loop  when one of
the two power loops  failed.   Each power loop could supply  the plant with  its
full operating  power requirement..   If  both  power loops fail,  the  stand-by
generators automatically  start.  The  plant standby  generator was  a  625   kva
diesel fuel powered  unit and  provided  the plant with only  part  of its   full
power requirement.  It had the  capability  of operating  the Thompson  River Lift
Station,  one  aeration blower,  the  return sludge  pumps,  the ozone  generation
system, and  other  supporting  equipment   to  provide   a minimum  of  secondary
treatment and disinfection.   The Fish  Creek Lift Station stand-by generator
was a 125 kva diesel fuel powered unit  and could  operate  all the pumps in  the
lift station.

Plant Laboratory
     The laboratory at the UTSD plant was expanded and equipped to conduct all
standard  microbiological  and wet  chemistry  analyses  conducted during  the

                                      41

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research effort.   The analyses  that  were conducted are  summarized in Appen-
dices A through F.  The laboratory was located in the main plant building in a
9.9 m (32.5  ft)  by 4.1 m  (13.5  ft)  room with total counter  length of 13.7 m
(45 ft).

Potable and Non-Potable Water Supply

     The plant  was designed with  its own potable  water  supply system.   The
system included  a shallow well  located near  the  plant  site,  a chlorination
unit, a pressurized storage tank, and a  pumping  system.   The well was located
near the Thompson River Lift  Station and  the chlorination  unit  and pumping
system was located in the  lift station dry-well.   Potable  water was  supplied
to the  plant laboratory,  restrooms,  ozone generation system,  filter control
system, and  raw  sewage pumps.   The system was capable  of supplying 2.5 I/sec
(40 gpm) of potable water at 413 k N/sq m  (60 psig) pressure.

     The plant  non-potable water  supply  system was  ozone contact  basin ef-
fluent, and  was  used for plant  washdown  and outside irrigation.   The system
consisted of a pressurized storage  tank and a pumping system.   The system is
capable of supplying  6.3 I/sec  (100  gpm)  of non-potable  at  461 k  N/sq  m (67
psig) pressure.
                                      42

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                                   SECTION 6
                           DATA COLLECTION PROCEDURES
    To evaluate the  individual  unit  processes  at the UTSD  facility an  exten-
sive sample collection and analysis  schedule  was  implemented.    However,  the
laboratory was only  partially functional  from  plant start-up  in  March  1976
until October, 1976, due  to equipment  delivery   delays   and  other   start-up
problems.  A limited analytical  schedule  was  followed  using the M &  1,  Inc.
laboratory located in Fort Collins,  Colorado  until  the full analytical  sched-
ule was implemented at the UTSD  laboratory.  As  closely as  possible a  similar
sample collection and analysis  schedule was maintained  throughout  the  project.
However, some modifications were necessary in order  to  allow for special test-
ing to be completed on various unit  processes  and to  conduct  quality control
checks.

Analytical Procedures and Quality Control

    The procedures used for data analysis  during  the  research project were
Standard Methods and/or EPA procedures with  minor modifications.    A listing
of the specific procedures for each  analysis and description of the modifica-
tions used is presented in Table 12.
                                      43

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      TABLE 12.  DESCRIPTION OF ANALYTICAL PROCEDURES  IMPLEMENTED DURING
                 RESEARCH PROJECT                       	
Analysis
         Procedure
                                                     Comment
BOD5
COD
TSS
TKN
NH4-N
Std. Methods, p. 543*
Std. Methods, P.550-554,
Std. Methods, p.94.
EPA Manual, p.159-163**
EPA Manual, p.175-181
N02&N03-N   EPA Manual,  p.201-206
Total P     EPA Manual,  p.251-255
Alkalinity   Std.Methods,  p.278-282
PH
Samples not seeded; in-bottle dilu-
tions made, 2 dilutions per sample run;
same bottle initial and final D.O.'s
made using an electronic D.O. meter.

20 ml aliquots used; standards of
potassium hydrogen phthalate run with
each set.

Gooch crucibles and glass fiber filters
used.

Micro procedure used; titrimetric or
Nessler finish used as necessary; Stan-
dard solutions of glutamic acid run
with each set.

Micro procedure used; titrimetric or
Nessler finish used as necessary; Stan-
dard solutions of ammonium chloride run
with each set.

10.0 mg/1 of N03~N used instead
of 1.0 mg/1 to achieve complete activa-
tion of cadmium-copper column.  This
alteration assured constant color de-
velopment.  Standard solutions run with
each set.

Persulfate digestion used; digested
samples neutralized with sodium hydrox-
ide to phenophthalien pink color  (not
to metered pH 7) then 5N sulfuric acid
added until pink color dissipated;
standard solutions run with each  set.

Potentiometric titration to pH 4.5;
Tris (Hydroxymethyl) aminomethane used
to standardize sulfuric acid titrant.

Orion 701 digital pH meter, calibrated
at pH 4 and pH 7 before each set  of
measurements.

                            (continued)
                                      44

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                             TABLE 12.   (Continued)
Analysis
      Procedure
                Comment
D.O.
Coliform
Std.Methods, p.922-925;
    928-935 and 937-939
YSI Model 54RC electronic oxygen meter
with field and BOD probe air calibrated
prior to each set of measurements.
MPN analysis used on ozonated samples;
membrane filter technique used on other
samples; two or more dilutions run on
each sample.
 *Standard Methods  14th  ed.,  1975, APHA,  AWWA,  WPCF.
**Methods for Chemical Analysis,  1972,  Environmental  Protection Agency.

    The  routine  analytical schedule incorporated  several quality control  as-
pects.   Routine  maintenance, cleaning  and  calibration of all  instruments  was
conducted.   Also, modifications were made  to some equipment to reach the  re-
quired performance  level  (i.e«,  special high altitude operating pressure  gauge
for the  autoclave and  special pretreatment  of influent to the  distilled  water
system).  Class A,  borosilicate  glassware was used for volumetric measurements
and was  washed with lab detergent,  rinsed with  tap  water,  rinsed  with dis-
tilled water and air dried;  or  acid  cleaned,  rinsed with distilled water,  and
air  dried.    ACS reagent  grade  chemicals  and high  quality  distilled   water
(specific conductance  less than  5 micromhos/cm)   were  used to  make  all rea-
gents, except for Nesslers reagent which was  purchased commercially.  Routine
duplicate analyses  and standard  samples, where applicable,  were conducted on
at least 10%  of  all analyses.   Special microbiological  samples were analyzed
by three laboratories:   the UTSD  lab, the M &  I lab and the Water Quality  lab
at Colorado  State  University.   The  quality  control  checks  conducted  on  all
duplicate,  standard, and  split  samples  indicated  that satisfactory techniques
were implemented and maintained at the  UTSD lab.
    All raw data were developed using bench cards and calculations were double
checked before recording the results on  the  weekly  data sheets.  Weekly aver-
ages of the data were then computed  and  were recorded on data summary sheets.
The weekly  average results  for  each  unit process  are presented  in process
                                      45

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sequence from  Appendix A through  Appendix F and  serve  as the basis  for  the
data evaluations made in this report.

Analytical Schedule and Sample Type and Collection Frequency

    To  aid in  sample identification  and analysis,  the  mainstream sampling
stations were numbered as shown in Figure  5.
FISH CREEK
LIFT STATION

CD ©
!
\

THOMPSON RIVER
LIFT STATION

                              FLOW EQUALIZATION
                                      J!
                               ACTIVATED  SLUDGE
                            [NITRIFICATION  TOWER |
                                    ©I©
                            MIXED MEDIA FILTRATION
                              OZONE  CONTACT  BASIN |
                               BIG THOMPSON RIVER
     *Note 5 - Sample when Redwood Media was used.
           6 = Sample when Dumped Plastic Media was used.
           7 = Sample during denitrification special study.
           8 = Sample during normal operation.
      Figure 5.  Mainstream sampling stations during the research project.
                                      46

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     During the course of the research  project  some  sample points were deleted
 and others  were  activated  during  the different  evaluation periods.   Sample
 station No.  2 (Fish Creek Lift Station) was  not  sampled  because of its remote
 location and because the flow from this lift station represented less than 10%
 of the flow to the plant.   Sample station No.  5  (Nitrification tower effluent
 - Redwood media)  and sample  station  No.  6 (Nitrification  tower  effluent  -
 Dumped media) were used  correspondingly when each of the different media types
 were evaluated.   Sample station No.  7 (Mixed-media Filter  -  Denitrification
 effluent)  was  activated  only during  the  methanol  addition/denitrification
 phase  of the research effort.   During all  other  times  of the  project  sample
 station No.  8  (Mixed media  filter  effluent) was  used.   Sample station No.  3
 (Flow  equalization basin effluent),  station No. 4 (Activated sludge effluent)
 and station  No.  9  (Ozone  contact  basin  effluent)  were  used  throughout  the
 research project.   Sample station No.  10 was not  used  for the routine research
 project results.

     Different types of  samples were collected  depending  on  the nature  of  the
 parameter  analyzed.  Grab  samples  and/or in-situ measurements were  used  for
 dissolved  oxygen,  pH,  fecal coliform,   total coliform and  temperature  measure-
 ments.    Composite  samples  were collected  for  the BOD^,   COD,  TSS,  TKN-N,
 NIfy-N,   N02&N03-N,   Total P and alkalinity  measurements.     The  composite
 samples  were collected  both automatically  and  manually.   Two  refrigerated
 automatic  samples  (Isco  Model 1580R)  were  used  to  collect  the  samples at
 sample  station  No.  1 (Thompson  River Lift  Station Influent)  and station No.  3
 (Flow  Equalization Basin Effluent).    The  automatic sampler  at station No.  1
 collected  the samples  proportional  to  flow through operation according  to  the
 number  of  lift  station pump  cycles.     The sampler at  station No.  3  collected
 equal volume  samples every 2 hours, and since the  flow rate from the equaliza-
 tion basin was  controlled at a  constant rate  throughout the day the sample  was
 collected  proportional  to flow.   The   daily  composite  samples were  collected
manually at  all other sample stations.  During the first  four months of  the
research project  (June  1976-September   1976)  composite  samples  were  collected
for a period  of 8 hours to 16 hours each day.   During the  remaining twenty-two
month  data  collection  phase  of  the  project,   equal   volume samples  were

                                      47

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collected at  2-hour intervals for  a 24-hour period.   Because the  flow rate
through  the  plant was  controlled at  a constant  rate,  the  composited equal
volume samples were proportional to flow.

    Composite samples were  collected  on Sunday  through Thursday and were ana-
lyzed  Monday through  Friday.   Grab  samples were  collected  Monday  through
Friday.  The analytical schedule that was followed is shown in Table  13.

          TABLE 13.  ANALYTICAL SCHEDULE FOR THE MAINSTREAM SAMPLES
Analysis
TSS
COD
TKN-N
NH N
N02&N03-N
Total P
Alk
Alk
BOD5
Coliform
(Tot. & Fecal)
Coliform
(Tot. & Fecal)
D.O.
PH
Temp
Frequency
5/wk
t*
"
it
••
ti
ii
2/wk
2/wk

2/wk

5/wk
5/wk
5/wk
5/wk
Sample Type
Composite
ti
ti
tt
tf
"
ii
It
tt

Grab

Grab
in-situ
Grab
in-situ
Sample
1





5
1
1

1

7
1
1
1
, 3





or
, 3
, 3

, 3

or
, 3
, 3
, 3
, 4





6,
, 4
, 4

, 4

8,
, 4
, 4
, 4
, 5





9
, 7
, 5

, 5

9
, 5
, 5
, 5
or






or
or

or


or
or
or
Station*
6,
tt
ti
it
11


8
6,

6,


6,
6,
6,
7 or 8,







7 or 8,

7 or 8,


7 or 8,
7 or 8,
7 or 8,
9









9


9
9
9
*1.  Thompson River Lift  Station  Influent.
 3.  Flow Equalization Basin Effluent.
 4.  Activated Sludge Clarifier Effluent.
 5 or 6.  Nitrification Tower Effluent - Redwood  or Dumped  Plastic Media.
 7 or 8.  Mixed Media Filter Effluent - Denitrification  Phase  or Normal Phase.
 9.  Ozone Contact Basin  Effluent.
    In October  1977,  the  analytical frequency for Total P and for COD was  re-
duced  to  2 and 3  times per week,  respectively,  based on  an analysis of  the
5-times per  week results.   The  analysis was made for  one  week of each month
for a  10-month period from December 1976 to  September  1977.   The analysis  of
the COD results compared the  data  for 5 days  to data for  3 days within  the
same week.   On  the  average  these values  were  within  1.5 percent  of each other.
                                      48

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 Similarily,  comparing the weekly results of Total P for the 5 days of analysis
 to  2  days of results showed that oil  the average these values were  within 2.0
 percent  of each other.   Reducing the analytical  schedule  enabled  the staff to
 devote laboratory  time  to special testing,  yet it did not  adversely affect the
 results  of the  data  collected.

    In addition to  analyses  of the  wastewater,  various  analyses  of the  in-
 plant sidestreams  were  conducted periodically.   The analyses  were  conducted on
grab  samples of waste  sludge,  aerobic  digester supernatant,  aerobic  digester
sludge,  dewatered  sludge,  activated sludge mixed liquor,  backwash  wastewater,
sludge dewatering  recycle,  and  river  samples.  The various analyses  conducted
included  BOD5,  TSS.  D.O.,    PH,  TKN,   N02&N03-N,   NH4~N,   Total   P,   COD,
ALK, Total Coliform,  Fecal Coliform,  SVI, and VSS.
                                     49

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                                  SECTION 7
                            RESULTS AND DISCUSSION
GENERAL

    Data  required for  the evaluation  of the  overall performance,  cost and
design aspects  of the  UTSD  treatment system and  for each  of  the individual
unit processes  was collected  for  a 105-week period.   The  effluent  from the
individual unit  processes was not  sampled  during the initial  and final por-
tions of  this 105-week  data  collection period.   Initial laboratory start-up
problems  postponed some  individual unit  process analyses  for  three  months
until 10/3/76.  During  the final portion   (i.e., last two months) of the data
collection effort,  special testing for the  ozone  and denitrification  systems
was accomplished  in place of  sampling and analyzing all of the unit processes.
Thus, of  the  105 weeks during which  overall performance  information was col-
lected, data was  collected on a routine basis for the  individual  unit process-
es for an 88-week period.  During  June  1977, the activated  sludge process was
removed from  service to  provide  modifications  to  the gates between the two
aeration  basins  and  the two  aerobic digesters.   No  data  was collected during
this period.

     In this  section of the report  the  evaluation of  individual unit  processes
is presented  as  they  occur  in the plant  flow  schematic, beginning  with the
flow equalization process.  Also presented are  the results of separate  special
studies conducted on the denitrification, ozonation and sludge dewatering sys-
tems.  Finally, an overall evaluation of  all processes is presented.
                                      50

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FLOW EQUALIZATION

    The flow equalization  process was  used  to  control  the  wastewater  flow rate
and the recycle  flow rates through the UTSD plant.   Wastewater was  pumped  to
the basin from both  lift  stations,  and  a controlled rate of  flow  was  dis-
charged from  the basin.   (All  in-plant recycle streams were  returned to  the
Thompson  River Lift  Station).   The  liquid volume in the basin would  typically
increase  during the day and  decrease  during the  night, corresponding  to waste-
water flow variations.  The  equalization  basin was not equipped with an  aera-
tion  or  mixing  system  to  keep solids  in  suspension,  although structural
provisions were made  if operating  conditions  warranted oxygen addition and/or
mixing.   As  designed,  however,  settleable solids  entering the  basin  would
settle to the  bottom of the  basin and were then scraped to the center of  the
basin where the discharge  pipe  was  located.   Provisions to handle  the organic
variations in  loading associated with this arrangement were provided in  down-
stream systems.

    These aspects  of the  flow  equalization  process that  were  evaluated  in-
cluded:

    a)  Affects of minimal mixing and  no oxygen  addition.
    b)  Characteristics of influent and effluent.
    c)  System operations and maintenance requirements.
    d)  Performance with respect to hydraulic dampening capability.

    Since minimal mixing and no oxygen addition were provided the  possibility
of low  D.O.  conditions and  odor problems  existed.   The   basin  influent and
effluent  D.O.  concentrations were  measured daily  for  a  one-year time period.
Figure 6  shows the 4-week average D.O. results throughout  the period  of inves-
tigation.   As  shown,  the  fall,  winter and spring influent and  effluent D.O.
concentrations were  above 1  mg/1.    The  summer effluent  D.O.  concentrations
were minimal (0.1 mg/1), but no  odor problems were experienced.  The  relative-
ly high D.O.  concentrations  during  the colder  periods  of the year were attri-
buted to  the relatively cold wastewater temperature (5°C to 6°C in  the winter)
and resulting  reduced  biological  activity in  the  equalization basin.   The
                                       51

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   !
   s
   >
         •J'A'S'O'N'D'J'F-M'A'M-J'J'A'S'O-N'P'J'F.M'A'M.J.J
         1976            1977                            1978
          Figure 6.  Flow equalization basin influent and effluent
                     dissolved oxygen concentration.
lower D.O. concentration  in the summer was attributed  to  a higher wastewater
temperature of about  18°C., which affected both the  soluability of oxygen as
well as increasing  the  biological activity.  The absence  of  odors during the
summer  was partially due  to  shorter basin  detention times  associated with
higher  summertime flow rates.   The  basin detention  time at.  one-half plant
design flow of 2,840 cu m/day (0.75 mgd) and  at a basin level of 1.8 m (6 ft)
is 5.2 hr.  During  the summer a  flow  of  2,840 cu m/day (0.75 mgd) was reached
and often  exceeded.   Another major reason  for minimal odors during the summer
was  attributed  to  the  fact  that the  settleable  organic  material  in  the
wastewater was removed from  the  basin  shortly after  it   entered,  much more
rapidly  than  the  average  hydraulic  detention time  indicates.   Thus, these
solids were not available to contribute  to  the biological  activity which could
produce odors.

    Other  than a  change in  the D.O. concentration,  no significant chemical or
biological changes in  wastewater  characteristics  occurred  within  the flow

                                      52

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 equalization basin.   A  summary of results  of  various parameters analyzed  in
 the  basin influent and effluent is shown in Table 14.
      TABLE  14.   SUMMARY OF -FLOW EQUALIZATION BASIN INFLUENT AND EFFLUENT
     _ CHEMICAL AND MICROBIOLOGICAL QUALITY* _
                                                                  Percent
                                                                 Difference
                              Basin
Basin
                                                                  Xi -
Parameter
BOD5 (mg/1)
TSS (mg/1)
COD (mg/1)
TKN (mg/1)
NH4-N (mg/1)
Alk as CaC03
Total P (mg/1)
Dissolved Oxygen
Total Coliform**
Fecal Coliform**
Influent (Xx)
218
200
351
20.6
12.6
109
5.5
(mg/1) 4.1
4.0 x 106/100 ml
1.1 x 106/100 ml
Effluent (X2)
213
180
330
22.4
12.9
108
5.8
2.6
4.6 x 106/100 ml
1.1 x 106/100 ml
\ *2 1
2.3
11.1
6.4
-8.0
-2.3
0.8
-5.2
57.6
-13.0
0
  *Summary of data from  11/28/76 to  12/24/77.
 **Geometric Mean.
    For  all  parameters analyzed  except  dissolved oxygen  and total  coliform,
the percent  difference between influent  and effluent ranged  from -8.0 percent
to 11.1  percent.   These differences  are felt to  be  within accepted sampling
and/or testing accuracy.   The total  coliform  difference  was -13 percent, but
the fecal coliform difference was negligible.  The difference in D.O.  concen-
tration  was  58 percent.   This change was attributed  to  biological activity
within the  basin,  but  as  mentioned earlier did  not  result  in  any odor pro-
blems.   The  flow equalization process was evaluated  for  one full  year of the
two-year data collection  phase of the research project.   Data collection was
then  stopped because chemical and  microbiological changes  through the basin
did not  appear to be  significant,  and  it was felt  that more  time  could be
devoted  to data collection for special studies and other process evaluations.

    The equalization basin was rectangular in  shape  and had an overflow side-
water depth of 3.66 m (12 ft).  The total  basin volume was 1,230 cu m (325,440
                                      53

-------
gal).  Typically,  the  basin operated between fill depths of  0.91  m and 2.7 m
(3 ft and 9 ft).  At the flow rates  experienced during the research project no
problems were  encountered  with basin capacity  respective  to sufficient stor-
age volume for flow equalization.  However, daily average flows  ranged  from 15
to 67  percent  of  design plant  flows.   The  flow rate  from the  equalization
basin was measured by  a magnetic flow measuring  instrument  (mag meter).  The
signal from the mag meter was used  to  indicate and totalize the flow rate and
also was used  to activate  the  flow  control equipment.   The  mag meter  signal
was sent to  a  controller assembly where  it was compared to  a  set  rate value
that was  "dialed" in  by the operators.    The  controller  would  then open or
close a "pinch valve"  to increase  or decrease the basin effluent  flow  rate as
called for.  This  system,  when  functioning, controlled  the flow rate from the
basin to +2 percent from the set rate which resulted  in  excellent  dampening of
the hydraulic flow.

     Some problems were experienced  with the  flow equalization process, mainly
in the area  of  flow  measurement and control  which  prevented the  system's use
on a  continuous basis.   Problems  included calibration  difficulties with the
mag meter  and problems  with the  mechanism  that  opened or  closed the pinch
valve.  The mag-meter  was  difficult  to  calibrate due to the lower  than design
flows that were received at the plant.   The meter was especially  difficult to
calibrate when flow  rates  were  only about  20  to  30  percent of design  values.
The pneumatically driven arm that  opened  and  closed the pinch valve had to be
pinched down quite substantially.    This  situation was  believed to have con-
tributed to  occasions of  improper  valve functioning.   Unlike  the  downstream
processes, the mag meter and flow  control valve were not provided  as parallel
trains and therefore were  sized based  on  total plant design flow.   During the
time the pinch valve assembly and mag meter were non-functional  an alternative
method of flow control was implemented.   This alternative method  consisted of
making routine adjustments  to a plug valve  located on the basin  effluent line.
The plant  flow variation using this method  of  control  was approximately +15
percent of  the desired flow rate.   It is  anticipated  that these  operational
                                      54

-------
problems  should  occur less  frequently  as  flow  increases, and  that  future
difficulties will be easier  to  correct  and/or  prevent  since  the operators have
gained more experience with  the system.

     During the flow equalization  evaluation period  a  grease build-up of about
13 mm to  25 mm (0.5 in to 1 in) occurred on  the basin walls.  This  build-  up
did not result in any  odor problems and  did not present an  aesthetic  problem
since the basin was covered.    Periodic  basin  cleaning  at  3-month  intervals
prevented  excessive grease build-up.   An operational  problem was  encountered
when the  scraper mechanism motor burned out.   With  the scraper not  operating,
slug loads of  settleable solids were directed to the  activated sludge  basins
when the  basin was  drained, down.   Flow  equalization  had  to be halted until the
motor was repaired.

GRIT REMOVAL

     The  grit  removal  system for  the UTSD system was designed with a  great
deal of flexibility to facilitate  grit and grease removal.   Because the  col-
lection system was  new, very little  grit  was  received  at the plant  site.  Air
was supplied  to the grit  basin to  aid in grease floatation.   However,  very
little grease accumulated  in the grit basin.   As mentioned, most of  the  grease
accumulated within the  flow equalization basin.   Within   the  grit  removal
building  slight odors could at  times be detected,  but  no  serious odor problems
ever developed.   In general,   the  grit removal  process  performed  in  a  very
satisfactory manner.

ACTIVATED SLUDGE

     The activated  sludge  treatment  process directly followed the flow  equali-
zation and grit removal systems.   With  this  arrangement all flow to  the  acti-
vated sludge process was equalized  prior  to  entry  to  the  process.   However,
the organic solids  loading was  not equalized  because of the  design  character-
istics of the flow equalization system.   Because  of the  flow equalization
                                      55

-------
design and the  fact  that no primary  clarifiers  were provided, all settleable
solids that were  received  at the plant were  received  in the activated sludge
aeration basins and eventually were wasted from  the  secondary  clarifier.  This
arrangement caused the  organic  loading to  the  system  to be  quite variable
within a day.

     Seasonal variations in hydraulic  and  organic  load  occurred  because the
plant served a  summertime  tourist oriented community.   The  flow to the  plant
during the research project  is graphically illustrated in Figure 7.  The  plant
organic load  as represented by  BOD5  is depicted  in Figure  8.    Flow  to the
plant during the  summer  of 1976  was  lower  than  the following tourist  seasons
because of the  Big Thompson flood  disaster  on July 31,  1976, which signifi-
cantly reduced  the community's  tourist trade.   The peak tourist season  lasts
about 3 months:   June,  July and August.   During  that  time the  flow  to the
plant was about 134 percent  greater than the  design flow.  (Note:   half  plant
design values  are used  for design  flow  because  only  half of  the activated
sludge units  were in service).    The BOD5  loading during  these  peak flow
periods was as much as 228 percent of design  values.  However, during the rest
of  the year  the  wastewater  flow and 8005  loading  averaged  about  50  percent
of design values.
     The  lower  BOD^  loadings  during  the  winter,  non-tourist  season were
caused by  lower wastewater flows  coupled  with relatively low BOD^  concentra-
tion of  about 100 mg/1  to 150 mg/1.   (See  weekly data  values presented  in
Appendix  B) .    These lower BOD^  concentrations were  attributed to  "bleeder"
water.   Bleeder water refers  to  tap water  that is  run  continuously to keep
water lines from freezing.  This  approach  is  used frequently  at  high altitudes
where deep ground  frost  is common and  where  dwellings are  not occupied full
time.  The significantly higher BOD5 loadings during the summer tourist sea-
son  were  caused  by higher  wastewater flows coupled  with  much  higher BOD^
concentrations  of 250 mg/1  to  400  mg/1.    The  higher  BOD5  concentrations
during the summer  were partially  attributed  to  a  small volume, high  strength
waste discharged into the UTSD collection  system  through a  septic tank  and
                                      56

-------
    O)
    E
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1.4
1.3
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1.1
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0.9
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0.4
0.3
0.2
0.1
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1976
1977
                                                        1978
Figure 7.  Plant  influent  wastewater flow rate during the research  project,
            (mgd x 3785 = cum/day)
          * Design flow for 1/2 of the activated sludge process in service.
     3200
     3000
     2800
     2600
     2400
                         DESIGN LOAD -x
         1976
1977
                                               1978
Figure 8.  Activated sludge  influent  BOD5  loading and effluent BOC5 residual
           (Ib/day x 0.454 = Kg/day)     "
          *Design loading for 1/2 of  the activated  sludge  process in service.
                                      57

-------
chemical vault dump  station.    As  such,  the flow  variation  throughout  the
project  (See Figure  7)  was not as  pronounced  as  the BODc;  loading.   (See
Figure 8).

     The treatment objective of  the activated sludge process was to reduce the
plant effluent  8005  concentration and to  facilitate ammonia oxidation in the
nitrification  tower.   However,  the  variable organic content  of the  influent
played an important part in the  system being able  to meet this objective.  To
evaluate the effect of the variable system loadings, the research results were
divided  into six different  operational  time  periods  (I  to VI) as  shown in
Figure 8.   In  Period  1 and IV,  low  BOD^ loadings  encouraged nitrification in
the activated sludge  system.   The influent ammonia loading and ammonia in the
activated sludge effluent is shown in Figure 9.   This  data  is also subdivided
into the six operational  time  periods.   In  Period III  and VI, extremely high
BODc loadings  for relatively  short  periods of  time caused excessive amounts
          J•A'S-O
         1976
N'D-J'F-M'A'M
    1977
J.J.A-S
D
• J • F. M-A•M- J • J
1978
   Figure 9.   Activated sludge influent ammonia loading and ammonia residual
               (Ib/day x 0.454 - Kg/day).
              *Design load for 1/2 of the activated sludge process in service.

                                      58

-------
of  8005  in the  activated sludge  effluent.   In  Period II and  V, relatively
low  BOD5  loadings  occurred,  but a  sudden  change  in  plant  BOD 5  loading
coupled with extremely  cold  wastewater  temperatures discouraged nitrification
in the activated sludge system.

     Period I and  IV are  characterized  by relatively  low  BOD^ loadings  and a
high degree  of  nitrification occurring  in the activated  sludge  process.   A
portion of the  results  for Period  I  were omitted  from  discussion because of
the Big  Thompson flood disaster  on 7/31/76.    After  the flood  the  plant was
seeded with sludge from the Estes  Park  Sanitation District.   The Estes Park
plant  was  nitrifying,  and the  nitrifying seed  sludge continued  to  convert
ammonia at the  UTSD plant.   Nitrification during  Period  I continued for 20
weeks  due  to the  relatively low  BODj  loading to  the activated  sludge pro-
cess.  Nitrification occurred for  16  weeks during  Period  IV  even  though BOD 5
loading was  higher, because  of  the  long mean cell  residence time that was
maintained in  the  system.   A  summary  of activated  sludge   performance for
Period I and IV is shown in Table  15.
            TABLE 15.  SUMMARY OF ACTIVATED SLUDGE PERFORMANCE FOR
                       OPERATIONAL PERIOD I AND PERIOD IV
Parameter
Flow (mgd)
BOD5
Influent (mg/1)
Effluent (mg/1)
Removal (%)
TSS
Influent (mg/1)
Effluent (mg/1) .
Removal (%)
TKN
Influent (mg/1)
Effluent (mg/1)
Period I
8/8/76 to 12/26/76
0.32

146
35
76

135
26
81

21
6.3
Period IV
9/4/77 to 12/25/77
0.39

260
31
88

224
30
87

26
5.3
                                      59
                                                             (Continued)

-------
                           TABLE  15.   (Continued)
Parameter
Nlty-N
Influent (mg/1)
Effluent (mg/1)
N02&N03-N
Influent (mg/1)
Effluent (mg/1)
Alkalinity (as CaC03)
Influent (mg/1)
Effluent (mg/1)
pH (median)
Influent (units)
Effluent (units)
MLSS (mg/1)
MLVSS (mg/1)
MCRT (days)
F/M BOD5/MLVSS (kg/kg/day)
Organic Load (Ib BOD5/day/
1000 ft3)
Clarifier OFR (gpd/ft2)
Period I
8/8/76 to 12/26/76
(20 weeks)
14
2.5
0.8
12
84
33
6.8
6.0
1670
920
9
0.21
12
255
Period IV
9/4/77 to 12/25/77
(16 weeks)
15
1.7
0.3
15
113
23
7.0
6.0
3730
2830
38
0.11
27
310
mgd x 3785 = cu m/day; Ib BOD5/day/1000 ft3 x 16
gpd/ft2 x 0.0408 - cu m/day/sq m
gm/cu m/day
     The average  effluent  ammonia  concentration during Period I was 2.5 mg/1.
This  resulted  in a  very  low  ammonia loading  to  the nitrification  tower.
Operational  controls  were  implemented to discourage ammonia  oxidation  in the
activated  sludge  system.   Increased  sludge wasting  was implemented to reduce
the  system mean  cell  residence time.  The  result was not effective  in dis-
couraging  ammonia  oxidation  and  had a  negative  effect on BOD5  removal,
which  was  only 76.0  percent.    Therefore,  in Period  IV (one  year  later)  no
attempt  was made to  discourage ammonia  oxidation with  operational changes.
                                      60

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 Extensive ammonia oxidation occurred  (effluent  ammonia concentration  was  1.7
 mg/1),  but BOD5 removal  improved averaging 88.1  percent.   The  organic  remo-
 val during these two operational periods was  satisfactory, but  high levels of
 ammonia oxidation affected  the  performance  of  the  nitrification  tower  dis-
 cussed  in a later  section.

     Organic loadings to the activated  sludge process were relatively low in
 Periods II and V;  however,  these periods were characterized by  limited nitri-
 fication in the activated sludge process.   Two factors were felt to be  respon-
 sible for the limited ammonia oxidation that  occurred.   At the onset  of  each
 of  these  periods  a  rapid  and  substantial  increase  in  both  hydraulic  and
 organic loading to the  plant occurred  due  to  a large  influx of  tourists during
 the  Christmas holiday season.   Wastewater  temperatures typically  decrease  to
 winter  time lows during this same period,  also.   Due to the influx of  people,
 the  BOD5 loading increased  during the start of Period  II  by  140 percent over
 the  4-week period prior to the holiday period.  At the start  of Period V,  the
 BOD5  loading  similarly  increased  by 141  percent.    This  increase  in  BOD5
 loading  and the associated  increase in sludge wasting appeared to  be directly
 associated with the  decreased ammonia conversion that occurred  in the acti-
vated sludge process.   After  the holiday  periods  loading  returned  to  the
 pre-holiday levels but nitrification  capability  did not reoccur.   It was felt
 that the low wastewater  temperature  of  only  4°C  to  5°C during  most  of  both
Period II and Period V discouraged  the return of the nitrifying organisms.  A
summary of  activated sludge performance  for  the  entire Period  II and Period V
interval is shown in Table 16.  The rapid changes in  the hydraulic  and organic
loading that characterized the beginning of each of these periods,  is shown in
the average weekly values presented in Appendix B.
                                      61

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            TABLE 16.  SUMMARY OF ACTIVATED SLUDGE PERFORMANCE FOR
                       OPERATIONAL PERIOD II AND PERIOD V
Period II
Parameter 12/27/76 to 6/12/77
Flow (mgd)
BOD5
Influent (mg/1)
Effluent (mg/1)
Removal (%)
TSS
Influent (mg/1)
Effluent (mg/1)
Removal (%)
TKN
Influent (mg/1)
Effluent (mg/1)
NH4-N
Influent (mg/1)
Effluent (mg/1)
N02&N03-N
Influent (mg/1)
Effluent (mg/1)
Alkalinity (as CaC03)
Influent (mg/1)
Effluent (mg/1)
pH (median)
Influent (unit)
Effluent (unit)
MLSS (mg/1)
MLVSS (mg/1)
MCRT (days)
F/M, BOD5/MLVSS (Ib/lb/day)
Organic Load (Ib BOD5/day/1000 ft3)
Clarifier OFR (gpd/ft2)
0.50

157
27
83

130
19
85

16.0
10.5

9
8

1.1
1.8

84
78

7.2
6.8
1495
1170
7
0.28
21
398
Period V
12/25/77 to 5/14/78
0.46

169
14
92

168
17
90

23.5
16.8

15
14

1.4
1.5

109
104

7.2
6.8
3720
2865
18
0.09
20
366
mgd x 3785 - cu m/day; Ib BOD5/day/1000 ft3 x 16 = gm/cu m/day;  gpd/ft2
x 0408 = cu m/day/sq m
                                      62

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      The fact  that nitrification ceased  is  common to  both  Period II  and V.

 The abrupt halting of nitrification in the activated sludge resulted in a sud-
 den increase  in ammonia  loading  to  the  nitrification tower,  which  impacted
 tower performance as described in a late section.


      Although many similarities existed between Period II and V, the activated
 sludge system was operated in a dramatically different fashion.  Since control
 of MCRT had not  produced  desired results during  1976,  it was  decided  to  try
 and improve organic removal capability during the winter of 1977.  As  a result

 the MLVSS  concentration was maintained 2.5 times  greater  during Period  V than
 during Period  II.    The  effect was  better  BOD5  removal during  Period  V,
 averaging  92 percent versus 83 percent BOD5  removal during Period II.


     Periods III and VI were characterized by dramatic  increases  in hydraulic
 and organic loadings associated with the  influx  of tourists during the  summer.
 A  summary of the  activated sludge loading  and performance  during these  periods
 is  presented in  Table  17.   As noted the  first  4 weeks of  Period  III are
            TABLE  17.  SUMMARY OF ACTIVATED SLUDGE PERFORMANCE FOR
            	OPERATIONAL PERIOD III AND PERIOD VI
  Parameter
    Period III
6/12/77 to 9/4/77
    Period VI
5/14/78 to 7/30/78
Flow (mgd)

BOD5
  Influent (mg/1)
  Effluent (mg/1)
  Removal (%)

TSS
  Influent (mg/1)
  Effluent (mg/1)
  Removal (%)
       0.91
        397
         89
         78
        271
        123
         55
                                      0.80
         310
          43
          86
         250
          20
          92
                                                                  (continued)
                                      63

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                            TABLE 17.  (Continued)
  Parameter

TKN
  Influent (mg/1)
  Effluent (mg/1)

Nlfy-N
  Influent (mg/1)
  Effluent (mg/1)

N02&N03-N
  Influent (mg/1)
  Effluent (mg/1)

Alkalinity (as CaC03)
  Influent (mg/1)
  Effluent (mg/1)
    Period III
6/12/77 to 9/4/77
        44
        28
        25
        24
         0.6
         2.0
       172
       144
                                                             Period VI
                                                         5/14/78 to 7/30/78
   26
   22
   17
  0.9
  4.5
151
116
pH (median)
Influent (unit) 7.2
Effluent (unit) 7.0
MLSS (mg/1) 3125
MLVSS (mg/1) 2270
MCRT (days) 5
F/M (Ib BOD5/lb MLVSS) 0.67
Organic Load (Ib BOD5/day/1000 ft2) 95
Clarifier OFR (gpd/ft2) 724
7.2
6.8
4103
3086
8
0.31
65.0
636
mgd x 3785 = cu m/day; Ib BOD5/day/1000 ft3 x 16 * gm/cu m; gpd/ft2 x
0.0408 = cu m/day/sq m
omitted because  the  plant  was  involved in a scheduled shut- down during which

time  modifications  were  made  to  the gates  separating the  aeration basins.
This  shut-down  required  reseeding  and  start-up  during  Period  III,  which

further hindered performance.
                                       64

-------
      The  BOD5  load  during Period  III  was  4.6  times  greater  than  during
Period  II.   Similarly, the  BOD5  load was 3.2  times  greater during Period  VI
than  during  Period V.  (Note:  Period VI  loading  was lower because the  Estes
Park  Sanitation District  flow was stopped on  June 1, 1978).   These increased
loadings occurred  over a three-month period,  and  no changes in  the activated
sludge  process  configuration  were  made.    (i.e., one-half  of the activated
sludge  process  units  were in service).   The  rapid  increase  in loading  resulted
in  reduced  process efficiency.   It should  be noted that  the loading  itself
and/or  process  operating parameters  like organic loading, F/M,  clarifier  over-
flow  rate; etc., were not  significantly high  in  themselves.   The main  aspect
that  led  to disrupted  performance  was  the  occurrence of  the higher loading
over  a  relatively  short period of time  and  associated  inability of the  acti-
vated sludge system to  quickly react.  This  aspect of a long time for  biologi-
cal  system  response  has  been further  supported  by  other  research.(2)     To
achieve satisfactory  performance  during the high  summer  loading period  it  is
necessary that  the UTSD plant staff allow sufficient time  prior to  the  peak
summer  loadings  to acclimate- the activated  sludge process  to handle  the  peak
loading conditions.

     Insignificant ammonia oxidation occurred  during  Period  III and Period VI.
This was felt to be due to  the relatively high organic loadings.  At  the  same
time  a  significant  increase  in ammonia  load  to   the  nitrification   tower
occurred.

NITRIFICATION
    The wastewater  directed over  the nitrification  tower consisted  of flow
received  from  the activated  sludge process  plus  flow  that  was recirculated
around the tower.  The maximum pumping volume to the tower was 22,710 cu m/day
(6 mgd), which provided a maximum recirculation capability of 4:1 at the plant
design flow rate.  The tower was divided into two equal volumes, each contain-
ing a different  type  of media.   The east side of  the  tower  contained plastic
dumped media which  had a specific  surface  area  of 89 sq m/cu m (27 sq ft/cu
ft).  The west side contained redwood media which  had a specific surface area

                                      65

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of 46 sq m/cu m (14 sq ft/cu ft).  In order  to approach design  loadings  on  the
media, only one half of the tower was operated at' any one  time; a  side by side
comparison of the two types of media was not possible.  During  the project  the
plastic media was  operated first and continued  through  September, 1977.   The
redwood media was then operated  for the duration  of  the project.

    Each media type was operated during three different phases  called:   start-
up, cold weather  and  warm weather periods.   The  separation point  between  the
cold weather  and  warm weather  periods  was  arbitrarily selected  as the poinj:
when the tower effluent  wastewater  temperature dropped below 8°C.  Using this
division point resulted  in a split of approximately 5  months of  cold weather
operation and 7 months of  warm weather operation  during a  one-year time  frame.
The start-up period for  each media type occurred  during a  warm  weather period.
Therefore,  during the two-year  data  collection  phase  of  the  research  effort
each  media  type was  operated  during a warm weather start-up  period,   a cold
weather operating  period  and a warm weather  operating  period.   These  operating
periods  are  labeled  plastic  start-up;  plastic cold  weather;  plastic warm
weather; redwood  start-up; redwood cold weather  and  redwood warm weather oper-
ation.

    After  the data  collection  phase  of  the research  project was completed,
additional  and  important data  was obtained  relative to the  performance  of  the
nitrification  tower.    Operation using  the   redwood media was continued,  and
some  warm-weather  and some  cold-weather  results  were   documented.    (Note:
These  results were obtained on  1  to 2-day  per week composite samples  as  op-
posed  to  5-day per week  composite  samples collected during  the research  pro-
ject.   Additionally,  only  a  portion  of the -analyses conducted during  the
project  were completed.    This  additional  evaluation was separated into  two
operational periods  called redwood update -  warm weather  and redwood update -
cold  weather.)
     Table 18  presents the  average  data  for  the selected  operational phases
 that were evaluated.  An  evaluation  of  this data is  presented  in the discus-
 sions of the  various operational phases.   It  is  important to note  that the
                                       66

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UTSD nitrification system was  designed to meet an  ammonia discharge limit of
54.8 kg/day  (120 Ib/day) which is  the  level that  was projected  to protect
against ammonia  toxicity in the Big Thompson  River  under  7 day,  10 year low
flow conditions.  This discharge limit would allow an effluent ammonia concen-
tration of 10 mg/1 at  the design flow rate of 5678  cu  m/day (1.5 mgd).   This
design  requirement  was  met throughout  the research  project.    However,  the
evaluation of  nitrification capability  presented  in this report  is based on
the  ability of  the nitrification process  to perform at  more constraining
levels  of effluent  ammonia concentration  (i.e.  >  2  mg/1  NH^-N)  and/or  at
greater than 90 percent ammonia oxidation across the tower.

    An  overall  summary of  the  nitrification results for  the  entire research
project showing mass of  ammonia applied  to  the tower and mass of ammonia con-
verted  to nitrate nitrogen  by the tower  is  graphically illustrated in Figure
10.  Also shown are the dates associated with  the various  operational periods.
The bottom line in the graph depicts  mass converted and not mass remaining in
the tower effluent.  As  shown, the mass  of ammonia applied was extremely vari-
able throughout the project, ranging  from less than 2.3 kg/day  (5  Ib/day) to
more  than 114 kg/day  (250   Ib/day).   The  low ammonia  loadings  were usually
associated  with periods where  nitrification  was  occurring in  the activated
sludge  process.  The high ammonia loadings occurred during  the  summer tourist
season.
    The  mass of  ammonia oxidized  also  varied substantially  throughout the
research  project.   Many operational  and  environmental factors contributed  to
this variability.   Low ammonia loading to the tower resulted because nitrifi-
cation occurred  in the activated sludge  process;  a rapid increase in ammonia
loading  occurred  during  the  Christmas  holiday  season  and  extremely high
ammonia loadings occurred during  the  summer  tourist  season.   In addition, dif-
ferent operational procedures were implemented as the project  progressed, the
major  change being in  the  amount  and  method of  maintaining  recirculation
around the tower.   Environmental  factors  such as wastewater  pH, alkalinity and
temperature  also contributed to  the  variability  of tower performance.   These
aspects are  discussed  for each of the operational  phases  evaluated.
                                      68

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                       69

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Plastic Start-Up (July  11,  1976  to  November 27,  1976 - 20 wks)

    Data collection  for the nitrification  tower plastic  start-up period began
on July 11, 1976, but was  interrupted on July 31,  1976,  when the Big Thompson
flood disaster  occurred.   Because  of  this interruption  the  data presented in
Table 18 for this period  includes only those results  after  the effects of the
flood were minimized (i.e.,  8/22/76 to 11/27/76).   The period ends on 11/27/76
when the  tower effluent  temperature  dropped  below 8°C.   During  the plastic
start-up period the  ammonia loading to the tower  was  minimal because nitrifi-
cation occurred in  the  activated sludge process.   The average ammonia loading
to the tower was  only 6.9 gm/day/cum  (0.43 Ib  day/1000 ft3),  or 6 percent of
the  design  loading of 109  gm/day/cum  (6.8.  Ib  day/1000  ft3).     This  low
loading limited the  development of nitrifying organisms  on the plastic media.
The variations in ammonia  loading and ammonia oxidation for the  plastic start-
up phase are graphically depicted in Figure 11.
       g
          6O
          SO
          40
          30
       <  20
          10
                      NH4<-N t »PLII
                              A
            14  21  28  4   11  18  25
                                                          PL: STIC
                                                         STAI
                                                            T-l '
                                      8   15  22  29  6  13  2O  27   3   1O  17  24
                                         SON
                                        1976
     Figure 11.  , Nitrification tower ammonia loading and ammonia oxidized
                  during the plastic start-up operating period.
                                       70

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     The  tower  operational procedure during the plastic  start-up  period was to
maintain a  fairly  high tower recirculation (R/Q)•ratio (average was 4.9).  The
corresponding  tower wetting rate averaged  52 1/min/sq m (1.28 gpm/ft2)  and
varied  from 39  to  56  1/min/sq m  (0.97 to  1.38  gpm/ft2).   During  the  other
operational periods the  R/Q  ratio  and associated tower  wetting  rates  were
generally decreased.    Initially,  the tower wetting  rate  was  quite  variable,
but  finally was controlled at a  more  constant  rate.   The  reasons  for  the
changes  in. R/Q and tower  wetting  rate are presented in  the  operational phases
where the changes  occurred.

     The  R/Q ratio  and  wetting rate was maintained at higher levels  during  the
plastic  start-up period because the  original  tower distribution system  could
not  evenly  distribute  a  low flow rate  over  the  media  surface.   At low  flow
rates it was  felt  that poor, distribution  resulted in  loss  of utilization  of
part of  the dumped media in the  upper portion of  the  tower.   Therefore,  the
system's  original  fixed  splash-plate nozzles were  replaced  with  a variable
flow splash-plate  nozzle, which automatically adjusted  themselves  to  provide
good distribution  at low  flow rates.  The  new nozzles functioned very satis-
factorily and provided  an even distribution of flow over the media  surface  at
low, as  well as  higher flow rates.  A summary of  the  significant events  that
occurred  during the plastic  start-up  period is presented in Table 19.
    TABLE 19.  SIGNIFICANT EVENTS DURING THE PLASTIC MEDIA START-UP PERIOD
   Date	-             '                       Event
July 11, 1976

July 31, 1976
August 22, 1976
October, 1976
Plastic dumped media section of tower placed into
operation.
Big Thompson Flood Disaster occurred.
Data collection subsequent to the flood initiated.
Replaced fixed splash-plate nozzles with variable
flow nozzles.
                                                           (Continued)
                                      71

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   Date
                            TABLE  19.   (Continued)
                                                      Event
August thru November,
1976

August thru November,
1976
Tower influent ammonia concentration quite  low due
to nitrification in the activated sludge  process.

Tower recycle (R/Q) ratio and wetting rate  were
high at 4.9 and 52 1/min/sq m (1.28 gpm/sq  ft),
respectively.
Plastic - Cold Weather  (November  28,  1976 to April 23,  1977 - 21 wks)


    The plastic cold weather  operating time period began when the tower efflu-
ent  wastewater  temperature  dropped   below 8°C.    Initially,  a low  ammonia
loading existed  and lasted for about 4 weeks, as  shown in Figure  12.   Then,
ammonia oxidation  ceased in the activated  sludge  process  and a higher ammonia
loading was  applied to  the tower  for the remaining 17 weeks  of  the  plastic
     £  40 _
     z
     ui
        30
     <  20
     <  10
                                                            PLASTIC
                                                         GOLD WEA
           1   8   15  22  29  5  12  19  "26  2   8  16  23  2   8   16  23  30  6  13  2O
    Figure  12.   Nitrification tower ammonia loading and ammonia oxidized
                 during the plastic cold weather operating period.
                                       72

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cold  weather operating  period.    A summary  of the  results  for  the  17-week
period  of  cold weather  operation  with a higher  ammonia loading  is  shown  in
Table 18.  The ammonia  loading  during  this  time period averaged 32 gm/day/cum
(2.0  lb/day/1000  ft^)  or  465  percent greater   than  during  the  start-up
period.  However,  this  loading  was still only about  30 percent  of the design
loading rate.

    Initially the  operational approach during the  plastic cold weather period
was to  maintain  a fairly high tower recycle  ratio (R/Q) of  about 2.8.  How-
ever, ammonia oxidation  began  to gradually decrease  from about  80 percent  to
30 percent.   It  was  felt that  higher  recycle rates were contributing  to tem-
perature losses in the tower, which in turn were contributing  to the  decreased
tower performance.   Therefore, the tower R/Q  ratio was reduced gradually from
a peak  of  2.8 to 0.   This  gradual reduction occurred  over  an 8-week  period,
and  no  recirculation  was  provided  for   another   8-week  period.    When
recirculation was  reduced  and  eventually stopped, nitrification performance
did not improve; in  fact,  ammonia removal further decreased  to  only about  20
percent.  This gradual  reduction in ammonia  removal  is illustrated  in Figure
12; which  depicts  the mass of  ammonia applied  and  mass oxidized during the
plastic - cold weather period.    Tower recirculation was  stopped  on 1/23/77,
and was not started until the week of  3/13/77.  During  that time the  amount  of
ammonia oxidized in the tower dropped  from 3.6 kg/day (8 Ib/day) to 2.3 kg/day
(5 Ib/day),  while  ammonia  loading  to   the  tower  remained fairly  constant  at
about 12.7 kg/day  (28 Ib/day).    It was concluded  that minimal recirculation
did not improve nitrification performance.
    During the week of March  13,  1977,  recirculation was again implemented at
an R/Q ratio of  about  1*5.   Subsequent to  this  change,  ammonia oxidation in-
creased from about 20 percent to 50 percent over a 5-week period, although the
tower  effluent  temperature also  gradually  increased from  4°C to  8°C.   It
appeared that by providing some recirculation ammonia oxidation capability im-
proved, but the benefits of recirculation alone could not be confirmed because
wastewater temperature also increased.  A summary  of the events that occurred
during the plastic - cold weather operating period is shown in Table 20.
                                      73

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    TABLE 20.  SIGNIFICANT EVENTS DURING THE PLASTIC - COLD WEATHER PERIOD
                                                     Event
   Date
11/28/76 to 12/26/76
(4 weeks)
12/26/76 to 1/1/77
(1 week)
11/28/76 to 1/22/77
(8 weeks)
1/23/77 to 3/19/77
(8 weeks)
3/20/77 to 4/23/77
Low ammonia loading to tower due to nitrification in
activated sludge process.
Ammonia oxidation in activated sludge process
ceased.
Ammonia oxidation performance decreased from about
80 percent to 30 percent, over which time tower
recirculation rate was gradually decreased from
about 2.8 to 0.
No recirculation provided, and ammonia oxidation
decreased from about 30 percent to 20 percent.
Recirculation provided at R/Q ratio of about 1.5;
tower effluent temperatures gradually increased from
about 4°C to 8°C; and ammonia oxidation gradually
increased from about 20 percent to about 50 percent.
Plastic - Warm Weather (April 24, 1977 to September 24, 1977 - 22 weeks)

    On  April 24,  1977,  the tower  effluent  temperature  above  8°C  and  the
plastic - warm weather  operational period began.   This operating period  con-
tinued until  the  redwood media  was placed on line on  September  25,  1977.   In
total, this  period  continued for 22 weeks but was  interrupted  for  2 weeks  in
order to  complete a scheduled  repair  to the  activated sludge aeration  basin
gates.  A summary of results during the plastic  warm  weather period is  shown
in Table  18.
    The ammonia  oxidation performance of the  tower  during the plastic - warm
weather operational  period  is  illustrated in Figure 13.  As shown,  the amount
of  ammonia  loading  and oxidation  increased  dramatically  from  4/24/77   to
6/18/77.   Two  important points are depicted  in Figure 13; the rapid  increase
in  the  amount  of ammonia oxidized  and the overall  maximum amount  of  ammonia
oxidized.  The amount of ammonia  oxidized increased  from about 17  kg/day  to 36
kg/day  (37 Ib/day to 80 Ib/day) within  a 4-week period,  which  relates to  a
0.73  kg/day/day  (1.6 Ib/day/day) increase.   This rate of  increase  in  ammonia
                                      74

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    "Figure  13.  Nitrification  tower  ammonia loading and ammonia oxidized
                during  the  plastic warm weather  operating  period.
oxidation capability is compared to the response of the redwood media.later in
the report.   A maximum  ammonia  oxidation capability  of  about  36  kg/day (80
Ib/day) was achieved.  A similar maximum ammonia oxidation also  occurred later
in this phase after a scheduled interruption occurred.  Ammonia  loading during
this  period  was  much  greater  than  the  maximum  oxidation  rate  that  was
achieved.   As such,  relatively poor  ammonia removal percentages were achieved
(i.e.  48  percent).  It  is  noted that  an oxidation  of 36 kg/day  (80 Ib/day)
represents an oxidation per unit volume in the tower of 93 gm/day/cu m (5.8 Ib
/1000  ft^/day).   The corresponding  oxidation  per  unit of media surface area
in  the tower was 1.03  gm/day/sq m  (0.21  lb/day/1000  ft2) of  media surface.
These values will be compared  to  the removal performance of the redwood media
later  in the report.
                                      75

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    During the  plastic  warm weather operational  period  problems  were encoun-
tered due to periodic extensive  sloughing  of solids from the tower.  Sloughed
solids plugged the mixed media filters  which resultd in shut-down of both the
filters and the nitrification  tower.   The tower had to  be  shut down since it
was an integral part of the mixed media pressure  filter  system.  These period-
ic shut-downs dramatically pointed out  the limitations of the mixed media fil-
ters to handle  periods  of  high solids  loss  from  the nitrification system, as
described later.

    It was originally felt  that  a  portion of the  sloughing problem was due to
the diversion of  raw wastewater  over the tower during  the  two week period in
June 1977 when  the gate structure between  the activated  sludge  aeration basins
was modified.   This  diversion  was  felt to have contributed to  the  development
of a greater mass of carbonaceous organisms that sloughed  off the tower when
the raw wastewater flow to  the tower ceased.  However, sloughing was occurring
prior to this time and continued after  the gate modification  for the remaining
11 weeks of the plastic warm weather evaluation period.  Flow  variations that
occurred in tower wetting  rates  was felt to be another  possible cause of  the
tower sloughing problem.  However, no direct correlation between wetting  rates
and sloughing could  be established from the  data.

    For  the 4-week  period  from 7/17/77  to 8/13/77 while  sloughing  occurred
periodically and  while  loading exceeded oxidation, the  amount  of ammonia oxi-
dized varied  from 34 to 39  kg/day (75 to 87 Ib/day).   This relatively  small
fluctuation could lead  to the  conclusion that the system had  reached  a consis-
tent and maximum ammonia oxidation  level.  However,  the  tower sloughing  and
periodic  shut-down  (maximum 1-day  duration at minimum  1-week intervals)  may
have hindered  the nitrification system's  ability to attain a  higher  level  of
ammonia  oxidation.   Despite the interference of  tower  sloughing,  it  was  felt
that  the data  indicated  that the  tower was  capable of  oxidizing a  maximum
fixed amount  of ammonia.   This  conclusion is  significant  in that  it  requires
                                                                     j
that design loading be based on the maximum expected ammonia  load  that  would
occur  for  an  average  daily or weekly period,  and not  be based on  yearly
                                       76

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average loading conditions.  A summary of the significant events  that  occurred

during the plastic •*• warm weather operating period is shown in Table 21.
       TABLE 21.  SIGNIFICANT EVENTS DURING PLASTIC WARM WEATHER PERIOD
   Date

4/24/77 to 5/21/77
(4 weeks)
5/22/77 to 6/18/77
(4 weeks)
6/19/77 to 7/2/77
(2 weeks)
7/3/77 to 9/3/77
                           Event

- Ammonia oxidation increased from 50 to 60 percent.
- Mass of ammonia oxidized increased from 25.7 lb/
  day to 34.3 Ib/day, while ammonia loading remained
  fairly constant at about 2.7 lb/1000 ft3/day.
- Tower recirculation ratio ranged from 1.0 to 1.6.*
- Tower wetting rate averaged 0.83 gpm/ft2 and
  ranged from 0.76 to 0.92 gpm/ft2.

- Tower ammonia loading increased four fold from 2.7
  to 11.3 lb NH3/1000 ft3/day.  (Note:  11.3 lb
  NH3/1000 ft3/day is 166% of design load).
- Ammonia oxidation decreased from 86 to 46 percent,
  but mass of ammonia removed increased from 34
  Ib/day to 80 Ib/day (i.e., rate of increase was
  1.6 Ib/day/day).
- Extensive sloughing of solids from tower occurred,
  which required shut-down of mixed media filters
  due to plugging.
- Tower effluent temperature increased from 10°C to
  15°C.
- Tower recirculation rate varied from 0 to 1.2 de-
  pending on flow rate.

Activated sludge aeration basin gates modified and
all flow from the grit removal basin
was diverted directly to the nitrification tower.

- Extremely high ammonia loading to tower occurred,
  ranging from 7.4 to 18.3 lb/1000 ft3/day, or
  109 percent to 269 percent of design.
- After a 2-week period to overcome the effects of
  raw wastewater being directed over the tower, the
  maximum amount of ammonia oxidized was about 80
  Ib/day while loadings were almost 3 times that
  value..  (Note:  80 Ib/day relates to 5.8 lb/
  day/1000 ft3 and 0.21 Ib/day/1000 ft2 media
  surface).
                                                                (continued)
                                      77

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                            TABLE 21.  (Continued)
     Date
                  Event
7/3/77 to 9/3/77
(Continued)
9/4/77 to 9/24/77
- Extensive sloughing of solids continued.
  Procedures were implemented to reduce the
  sloughing, including maintaining a nearly
  constant hydraulic load on the towers, and were
  met with only moderate success.
Ammonia oxidation in activated sludge process reoc-
cur red.
Ib/day x 0.454 = kg/day; lb/day/1000 ft3 x 16.0 = gm/day/cum; gpm/ft2 x
   40.7 - I/day/sq m
lb/day/1000 ft2 x 4.88 = gm/day/sq m

Redwood - Start-Up (September 25, 1977 to November 19, 1977 - 8 weeks)

    On September  25,  1977  the  redwood media was  put into operation  and the
plastic media  was  removed from  service.   This change  involved  adjusting the
proper valves  to divert the influent to the other half of the tower.  The red-
wood  start-up period  lasted for  8 weeks
until  11/19/77,  when  the  tower effluent
temperature dropped below 8°C. During  this
time  a negligible  amount  of  ammonia was
directed  to  the  tower due  to nearly  com-
plete  nitrification that was    occurring
in  the  activated  sludge  process.    The
ammonia  loading  during the  first  week of
start-up  was   59 gm/day/cum (3.67 Ib/day/
1000  ft3).    But,  the ammonia  loading to
the  tower for the entire  phase averaged
6.4   gm/day/cum   (0.4   lb/day/1000   ft3)
because  less  than  1.6  gm/day/cum (0.1 lb/
day/1000  ft3)   occurred for 7  weeks of
the  8-week start-up  period.    These low
loadings  limited   the  development  of  a
nitrifying  population.   A  summary  of the
results  during the  redwood  start-up  period
                     >>
                     •
                     •o
                     111
                     O
                     O
                     tc
                     o
                     X
                        20
                        10
                                     1977
                      Figure 14.   Nitrification tower
                      ammonia loading and  ammonia ox-
                      idized during the redwood start-
                      up weather operating period.
                                      78

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 is  shown in  Table  18, and  a  graphical illustration  of  NH^-N load  and  Nlfy-N
 oxidized is  shown in Figure  14.

 Redwood  - Cold  Weather (November 20,  1977  to April 22, 1978 - 22 weeks)

    The  cold weather  period using  the redwood media  began on  11/20/77,  when
 the tower effluent temperature  dropped below 8°C«  The lowest  weekly  average
 wastewater  temperature during the  22-week time  period  was 3°C, and occurred
 for 2  separate  one-week periods. During the first 5 weeks  of the cold  weather
 operational  period,  minimal tower  ammonia  loading  existed because  extensive
 nitrification occurred in the  activated sludge process.  High organic  loading
 and low  temperatures which occurred over the Christmas holidays  caused nitri-
 fication in  the activated sludge process to  cease,  and  for the  next 17  weeks
 the  redwood  tower  was  loaded  at  an  average  level  of  59  gm/day/cum  (3.7
 lb/day/1000  ft^)  which was  54 percent  of  the design  loading  rate.   The  fol-
 lowing discussion about  redwood -  cold weather  operation  includes  data  col-
 lected during the  17-week time period  only.   A summary of the results  for  the
 17-week  period  is shown  in Table 18.
    The  increase in  tower  ammonia loading  began on  12/25/77,  and  continued
throughout the remaining  17 weeks  of  the cold weather  operational  time  period.
A graphical  illustration of  the  amount of  ammonia  applied to  the tower  and
amount oxidized  in  the  tower  for  the redwood cold weather  period is shown  in
Figure 15.   As shown, negligible  ammonia  oxidation occurred  for  the first  2
weeks.   Subsequently,  a gradual  increase  in ammonia  oxidation  occurred to  a
maximum  level  of 9.1 kg/day  (20  Ib/day),  which was  about 45%  of the  tower
loading.  The increase in ammonia  removal to 20 Ib/day occurred  over  a  15-week
period, for an average increase of 0.077 kg/day/day (0.17 Ib/day/day).

    The maximum oxidation level of 9.1  kg/day  (20 Ib/day)  was better than was
obtained during  the previous  year when the  plastic media was  operated.  Dif-
ferent operational  procedures may have  contributed  to  this  occurrence.  The
most important operational  change was in the tower  recirculation ratio.  The
R/Q ratio during the plastic  cold weather  operation  was  always quite low, and

                                      79

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    80
    70
    60
                  REPWOOD
                COLD WEA.THER
•i   *  :"   !   '  -M	r-
      83  30   7   14  21  28  4  11  18  25  1   8  15  22  1   8
    Figure 15.  Nitrification  tower ammonia loading and ammonia oxidized
                during the redwood cold weather operating period.

was eventually reduced to zero during most  of  the  period.   Conversely,  the R/Q
ratio during  the redwood cold weather operation  was substantially higher  at
2.5.  It appeared that a higher  recirculation  ratio improved ammonia oxidation
performance  during  the  cold  weather  operation.    During the  first  winter
(Plastic Cold Weather Period) it was felt that recirculation would  possibly
reduce the wastewater temperature and adversely affect ammonia oxidation capa-
bility.  However,  during the  redwood  cold weather  period  with recirculation,
the temperature  drop through  the tower  averaged  1°C.   A  similar  temperature
drop occurred during the  plastic cold weather  period when negligible  recircu-
lation was provided, thus a  significant effect of  high recirculation on waste-
water temperature was not observed.
                                      80

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     The better cold weather tower  performance  using the redwood media  may be
 attributed to the type of media  itself.   Possibly, the rough  surface  texture
 of  the  redwood as compared  to  the plastic  material enhanced growth  attachment.
 However,  because  of  the differences  in  the recirculation ratio during  each
 period  and because of  the  indication  that  a  higher  recirculation ratio  im-
 proved  ammonia oxidation capability, no definite  conclusions can be drawn as
 to  which media type performed  better during cold weather operation.  Also, no
 definite conclusion can be  drawn about overall cold weather  tower  performance
 because a  limited  population  of nitrifying organisms  was  established  during
 start-up.   Additional  information regarding cold weather  operation  for  the
 redwood media was collected after  the data collection  phase of the research
 project was  concluded.    In  this case, good pre-cold  weather start-up  condi-
 tions  existed.   A summary  of  the significant events  for  the  redwood  cold
 weather period is  shown  in Table  22.
      TABLE 22.  SIGNIFICANT EVENTS DURING REDWOOD - COLD WEATHER PERIOD
   Date
11/20/77 to 12/24/77
(5 weeks)
12/25/77 to 12/31/77
(1 week)
12/25/77 to 4/22/78
(17 weeks)
                         Event
  Negligible ammonia loading to tower due to exten-
  sive nitrification in activated sludge process.
  Nitrification in activated sludge process ceased.
- Tower ammonia loading averaged 3.7 lb/
  day/1000 ft3 or 54 percent of design loading.
- Ammonia oxidation increased from 4 to 47 percent.
- Negligible ammonia oxidation occurred during first
  2 weeks (i.e., about 2 Ib/day).
- Gradual increase in ammonia oxidation occurred
  over next 15 weeks to a maximum level of 20 Ib/day
  (i.e., average 0.17 Ib/day/day increase).
- Tower recirculation ratio averaged 2.5 and tower
  wetting rate averaged 0.98 gpm/ft2.
lb/day/1000 ft3 x 16 = gm/day/cum; Ib/day x 0.454 = kg/day; gpm/ft2 x 40.7
= 1/min/sq m
                                      81

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Redwood - Warm Weather   (April  22,  1978 to July 29,  1978 - 14 weeks)

    On  April 23,  1977,  the  tower  effluent  wastewater  temperature increased
above 8°C,  which marked the  beginning of  the redwood warm  weather operating
period.   A   summary of  the results  for the  redwood warm  weather operating
period  is  shown  in Table 18 and Table 23.   The results  shown  in  Table 23 are
separated  into  two 7-week periods,  one representing the  time  period when the
loading was  below the design level and the second when the load was above the
design  level.

    A graphical  illustration  of  the  ammonia loading and  ammonia oxidized in
the  redwood warm weather  period  is  shown  in Figure  16.    As  shown, ammonia
oxidized  through the tower gradually  increased from about 10.4 to  19.5 kg/day
(23  to  43 Ib/day)  from  4/23/78 to  6/10/78  (7 weeks), for an  average rate of
increase  of 0.18 kg/day/day 0.08 kg/day/day  (0.40  Ib/day/day).  This  rate was
2.4  times greater than the  rate  of  increase  that  occurred  during the cold
                  180
                  160
                -  140
                • 120
                  100
                   80
                O
                a
                   60
                   40
                   20
                                               REDNIOOD
                                             WAFM WEATh
                                             -Nf
                                             OXI 3IZE
                                                     ER
                                                  APPI IED
\
                     26  3   10  17  24  31   7   14  21   28  5  12  19  26
                      AM             J             J
                                      1978
     Figure 16.  Nitrification tower ammonia loading and ammonia oxidized
                 during  the redwood warm weather operating period.
                                        82

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weather   period   (i.e.,  0.81  versus   0.08   kg/day/day  (0.41  versus   0.17
lb/day/day)),  but was  not  as good  as  occurred  for  the plastic  media.    The
plastic  media increased its  ammonia  oxidation  rate  during  a  similar  time
period for the previous year an average 0.73 kg/day/day (1.6 lb/day/day).   It
appeared  that  the plastic media  provided a more  rapid response to  increased
ammonia  loading   during warm weather.    Also,  the maximum  level  of  ammonia
oxidized  by  the plastic media at  about  36 kg/day (80 Ib/day) was greater  than
the maximum  level oxidized by the redwood media.   The  average  mass of  ammonia
oxidized  by  the  redwood media for  the  7-week period  from  6/11/78 to  7/29/78
was  about '23  kg/day (50  Ib/day).    Thus, the  plastic media  responded  more
rapidly to a higher  tower loading and performed at  a greater  ammonia  oxidation
level than  the redwood media.  A possible reason  for  this occurrence may  be
due  to  the increased surface area of  the plastic media  at 88  sq  m/cum  (27
ft2/ft3)  as  opposed to  46   sq  m/cum  (14 ft2/ft3)  for  the  redwood media.
These dry specific surface area values  exclude the surface area attributed  to
growth on the media  which would increase both values  by an unknown amount.  A
comparison of  the maximum  unit oxidation  rates for each media shows that  the
plastic material  oxidized a  maximum  1.03 gm/day/sq m  (0.21  Ib/day/1000  ft2)
of media  surface  and the redwood  material removed  a  maximum 1.27 gm/day/sq m
(0.26 Ib/day/1000 ft2)  media surface.   According  to  these  values the  redwood
media oxidized about 20 percent  more ammonia per  unit of  surface  area, but
overall the plastic  media oxidized more  ammonia because it  had  52 percent  more
total media surface  area.
    The indication from the comparisons of media performance  is  that  the  plas-
tic media  had better  overall ammonia  oxidation capability  than the  redwood
media.   However,  the  plastic  media was being  loaded at a much higher  level
when its maximum ammonia  oxidation occurred  (i.e. ,  at an average 218 gm/day/-
cum  (13.6   lb/1000  ft3/day)  versus  147  gm/day/cum  (9.2  Ib/day/1000  ft3).
This higher loading may have  caused the plastic media to remove more ammonia.
However, ammonia  oxidation capability  may not  be  the  only  factor  that in-
fluenced media performance,,    During  the  redwood  warm weather operational
period minimal sloughing  of solids occurred, unlike  the problem with  routine
solids  sloughing  during  the  plastic warm weather  operating period.   During

                                      83

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     TABLE 23.  SUMMARY OF RESULTS DURING REDWOOD WARM WEATHER PERIOD
                (APRIL 23, 1978 TO JULY 29, 1978)
4/23/78 to
Parameter 6/10/78
Number of Weeks
Flow (Q) (mgd)
Recirculation Flow (R) (mgd)
Recirculation Ratio (R/Q)
Tower Wetting Rate (gpm/f t2)(min)
(Av.g)
(max)
Ammonia Nitrogen Loading
(lb/ day/1000 ft3)
BOD Loading (lb/day/1000 ft3)
Temperature Influent (°C)
Effluent (°C)
Ammonia Nitrogen Influent (mg/1)
Effluent (mg/1)
Removal (%)
Total Kjeldohl Nitrogen
Influent (mg/1)
Effluent (mg/1)
Nitrite plus Nitrate Nitrogen
Influent (mg/1)
Effluent (mg/1)
pH (median) Influent (units)
Effluent (units)
Alkalinity Influent (mg/1)
(as CaC03) Effluent (mg/1)
7
0.74
0.62
0.84
0.78
0.96
1.15
4.8
9.0
10
10
11
5.9
45
14
8.0
2.0
6.9
6.6
7.1
105
62
6/11/78 to
7/29/78
7
0.76
0.53
0.70
0.80
0.91
1.12
9.2
22
15
15
20
12
39
23
19
5.3
11.0
6.7
7.1
123
69
4/23/78 to
7/29/78
14
0.75
0.58
0.77
0.78
0.94
1.15
7.0
16
13
13
15
9.1
41
18
14
3.7
9.0
6.6
7.1
114
65
mgd x 3785 - cum/day; gpm/ft2 x 40.7 = 1/min/sq m; lb/day/1000 ft2 x
16.0 - gm/day/cum
                                   84

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each media  type's warm weather  operation condition, similar hydraulic wetting
rates were  experienced (i.e.,  redwood -  38 1/min/sq m  average and  32  to  47
1/min/sq m  variation  (0.94 gpm/ft2   average   and   0.78   to    1.15   gpm/ft2
variation)  versus plastic - 3.9  1/min/sq m  average and  27  to 48  1/min/sq m
variation (0.95 gpm/ft2 average  and 0.66 to  1.18 gpm/ft2  variation).   The
reason for  sloughing  from the plastic  media and negligible sloughing from  the
redwood media was not known.  The  problem with  the periodic solids  sloughing
by the plastic media was not that  it significantly reduced ammonia  oxidation
performance, but rather that it  plugged  the mixed  media  filters and required
system shut-down and bypass.  This  condition  could  have  been avoided by using
a different solids capturing unit,  like a clarifier.

    An important conclusion for both types  of media was that an apparent maxi-
mum ammonia oxidation rate was achieved.  The removal  rates achieved possibly
could have been improved by further  optimizing  operational adjustments,  but
the data indicates that some maximum oxidation level would  be achieved.    As
such, nitrification towers should be  sized  on  the  anticipated peak  daily  or
peak weekly ammonia loading, and not on an  average yearly value.  A summary  of
the events that occurred during the redwood warm weather  operating  period  is
shown in Table 24.
       TABLE 24.  SIGNIFICANT EVENTS DURING REDWOOD WARM WEATHER PERIOD
   Date
                                                 Event
4/23/78 to 6/10/78
(7 weeks)
- Tower ammonia loading was gradually increasing,
  but was less than the design loading (i.e., varied
  from 3.4 to 6.5 lb/1000 ft^/day or from 50 to
  96 percent of design load).
- Ammonia oxidation percentage remained constant at
  about 45%.
— Ammonia oxidation level increased as ammonia
  loading increased and ranged from 20 Ib/day to 43
  Ib/day.  (Rate of increase was 0.47 lb/day/day).
- Tower hydraulic loading averaged 0.97 gpm/ft2
  and varied from 0.78 to 1.12 gpm/ft2.
                                                           (Continued)
                                     85

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                            TABLE 24.  (Continued)
   Date
                     Event
6/11/78 to 7/29/78
(7 weeks)
Minimal sloughing problems were encountered.
Tower recirculation ratio varied from 0 to 1.9 as
flow rate varied.
Tower effluent temperature increased from 8°C to
12°C.

Tower loading averaged 9.1 lb/1000 ft3/day and
varied from 7.7 to 10.8 lb/1000 ft?/day, which
was an average 134 percent above design load and
varied from 113 to 159 percent above design
loading.
Average ammonia oxidation rate was about 40%.
Maximum ammonia oxidation reached 69 Ib/day for a
one-week period, but was variable and averaged
about 50 Ib/day for the 7-week period.
Tower wetting rate averaged 0.92 gpm/ft2 and
varied from 0.80 to 1.12 gpm/ft2.
Tower recirculation ratio averaged 0.71 and ranged
from 0.54 to 1.08.
Minimal solids sloughing problems were, encount-
ered.
lb/day/1000 ft3 x 16.0 = gm/day/cum; Ib/day x 0.454 = kg/day; gpm/ft2 x
40.7 - 1/min/sq m


Redwood Update - Warm Weather  (October 22, 1978 to November 18, 1978 - 4

weeks)


    Subsequent to  the  data collection phase of  the  research project, limited

but important information was developed regarding nitrification tower perform-

ance as  shown  in Figure 17.   The  most important fact was  that  the tower was
loaded at  a higher ammonia  level  prior to  cold weather conditions  than was

achieved during  the  previous 2  years.   The  average  tower  loading was  26

gm/day/cum  (1.6  lb/day/1000  ft3),  whereas  loadings  of  only  1.6  and  6.4
gm/day/cum  (0.1  and  0.4 lb/day/1000  ft3) were  achieved  in  1977 and  1976,

respectively.  The loading of 26  gm/day/cum (1.6 lb/day/1000  ft3)  was  about

24 percent of design.  At that loading during warm weather operation the tower
was  achieving nearly complete  ammonia  oxidation.    A  complete  summary  of
                                      86

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results for this time period is  shown  in Table 18.  As shown, the average  am-
monia oxidation percentage was 94 percent.  Therefore,  unlike  the previous  two
years the tower was receiving ammonia  and was  nitrifying  prior to cold weather
operation.   The  ammonia loading  to  the nitrification  tower  was increased  by
preventing  nitrification in the activated sludge process.    This  was accom-
plished by  substantially reducing  and  maintaining  a  low  D.O.  level.   D.O.
levels less than 0.5 mg/1 were maintained in the aeration basin  whereas levels
of 2-4 mg/1 were maintained  during the  previous  two  years.   This operational
change  increased  the  ammonia  loading  to  the  tower,  but  more  importantly
allowed the tower to become acclimated for nitrification  prior to cold weather
operation.

Redwood Update -  Cold  Weather   (November  20,  1978 to  February  24,  1979  -  14
weeks)

    On 11/20/78, the tower  effluent temperature dropped  below 8°C.   As  shown
in Figure 17, from  11/20/78 until 12/24/78,  ammonia oxidation rate was excel-
lent.  The oxidation rate varied  from  90 to 95 percent.  Between 9.1 and .13.6
kg/day (20  and  30  Ib/day) of ammonia  were  removed and the  tower  loading  was
about 24  to 35  gm/day/cum (1.5  to 2.2  lb/day/1000  ft3)  or  22  to  32 percent
of design.  For two weeks from  12/26/78 and  until 1/3/79, the.ammonia loading
more  than doubled  to  36  kg/day  (80   Ib/day)  due to  the  Christmas tourist
season.   During that time  the  amount  of ammonia  oxidized increased from 13.6
to 18.2 kg/day  (30 to  40  Ib/day), but was  only  50  percent  of the influent
loading.  The tower was  not  able to quickly respond  to the  rapid increase  in
ammonia loading  over  the 8-day  Christmas holiday period.    It  was concluded
that the  tower must be  previously acclimated  to  these peak loading conditions
in order  to be able to oxidize  the  increased  amount  of ammonia at the expectd
higher loading conditions.
    After  the  Christmas  holiday season  the tower  loading again  dropped to
about 13.6 to 18.2 kg/day (30 to 40  Ib/day).   At these loadings the tower am-
monia oxidation was about 10.9  to  14.5  kg/day (24 to 32 Ib/day), which repre-
sented an 80 percent removal.  This level of ammonia oxidation was better  than
                                      87

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         100
            REDWOOD  UP 3ATE
            WARM WEATHER
            18  25  1   8  15  22  29   6   13  20  27  3  10  17  24  31   1   14  21  2«
 Figure 17.  Nitrification  tower  ammonia loading and ammonia .oxidized during
             the redwood update warm weather and redwood update cold weather
             operating periods.
the two  previous cold weather  seasons, but  was reduced  from the 90  percent
that occurred prior  to  the Christmas holiday season.   The 80  percent  ammonia
oxidation rate continued for  3  weeks from 1/7/79 to 1/27/79.   Then,  extremely
cold weather occurred  and  the  tower  effluent  temperature  dropped to  1°C.
Subsequently, tower  ammonia oxidation gradually decreased from 80 percent  to
50 percent,  and  only about 6.8 to 9.1 kg/day (15 to  20 Ib/day of  ammonia was
oxidized.   It  is interesting to  note that this  level  of ammonia  removal was
similar to that obtained during the  redwood  cold weather  operational  period of
the previous winter.  A summary  of  the results  for  the  redwood cold  weather
period is shown in Table 18.
                                      88

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    The  updated  information for  cold  weather tower  operation indicated  that
initially,  better  ammonia  oxidation  existed  when  the  tower  was  properly
acclimated prior  to the cold weather  season.   However,  tower performance was
affected by  the  cold weather and  the  tower oxidation rate  decreased from 90
percent  to 50  percent  of the influent load.  During  this time,  similar  tower
recirculation ratios and wetting  rates existed  at about  2.0 and  35 1/min/sq m
(0.86  gpm/ft2),   respectively,  as  existed during  the  previous  cold-weather

period  (i.e.,  2.2  and 40  1/min/sq m (0.98 gpm/ft2)).   The  tower  effluent
temperature ranged  from 8°C  to as  low  as  1°C to 2°C.  These  lower temperatures
were 1°C to 2°C colder  than  previous winters  due  to a much  colder than normal
winter.  It was concluded that even if the  tower  was  acclimated,  a significant
cold weather effect does  exist  at the relatively cold wastewater temperatures
experienced at the  UTSD plant.   A summary  of the events that occurred during
the redwood update  cold weather period is shown in Table  25.
  TABLE 25.  SIGNIFICANT EVENTS DURING REDWOOD UPDATE - COLD WEATHER PERIOD
   Date
                   Event
11/20/78 to 12/24/78
(5 weeks)
12/24/78 to 1/6/79
(2 weeks)
1/7/79 to 1/27/79
1/28/79 to 2/24/79
(4 weeks)
Ammonia oxidation varied from 90 to 95 percent.
About 30 Ib/day of ammonia was removed.
Tower loading was about 2.2 lb/day/1000 ft3 or
32 percent design.

Tower loading rapidly doubled to 80 Ib/day
(i.e., 5.8 lb/day/1000 ft3 or 85 percent
design).

Tower loading decreased to 30 to 40 Ib/day
(i.e., 2.2. to 2.9 lb/day/1000 ft3, or 32
to 43 percent of design).
Ammonia oxidation was about 80 percent.

Tower loading remained at 30 to 40 Ib/day.
Tower effluent temperature varied from 1°C
to 3-°C (colder than previous two winters).
Ammonia oxidation decreased from 80 to 50
percent.
Ib/day x 0.454 = kg/day; lb/day/1000 ft3 x 16.0 = gm/day/cum
                                      89

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Overall Nitrification Evaluation

    Nitrification tower  performance as compared  to  a >  90  percent oxidation
capability was  marginal throughout  the research  project,  except  during the
fall and early winter of 1978, when 90 to 95 percent ammonia oxidation existed
and  the  tower loading  was about  32 percent  of  its  design value.   Several
events occurred during various  times of the research project that contributed
to the tower's  low overall ammonia  oxidation efficiency.   Among these were:
negligible tower  loading  during  start-up,  rapid  increases  in  tower  loading
during cold weather  operation,  summer loadings on one half  of  the tower that
were significantly greater than design,  periodic  sloughing of solids from the
tower  which  necessitated  periods  of shutdown,  varying  tower   recirculation
ratios, and low wastewater temperatures during cold weather  operating periods.
In addition to  these items several other factors  were felt  to be potentially
detrimental to ammonia  oxidation capability of the tower; low pH and alkalin-
ity.  Controlled bench  studies  were conducted to  test the potential impact  of
these items on the ammonia oxidation capacity  of  the UTSD plant.

    The results of the bench  test  special studies  showed  that given  sufficient
time,  complete  nitrification always  occurred.  When alkalinity was added and
the  pH was increased,  the rate of  ammonia oxidation increased  substantially
and  complete  nitrification eventually occurred in all batch tests.  It  should
be noted that the optimum  pH  for  nitrification is  above  neutral  (approximately
pH 8.6).   The pH of  the  tower influent  was  always  on the  acid  side  of neutral,
and  ranged from pH 5.8  to  pH  6.8.

     From these bench scale studies it was concluded  that  the full scale  nitri-
fication results  during the research project  could have  been dramatically  in-
fluenced by low wastewater pH.   It was hypothesized that the lower  overall  pH
values hindered the rate  of  ammonia oxidation capability through  the  towers,
and  sufficient  time and/or exposure to the nitrifying microorganisms was  not
available  to achieve good  nitrification   at  the loading  rates  experienced.
This hypothesis could not  be confirmed  during the research project.
                                      90

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    Under  present  loading conditions it may  be  necessary to place  the  entire
tower  (both the redwood and  plastic  media)  into  service  to  achieve  better
ammonia oxidation  capability.   In so doing increased contact time with  nitri-
fying  microorganisms would  be attained which would overcome  the  documented
nitrification  rate reducing effect of  the  low wastewater temperature and  the
hypothesized nitrification rate reducing effect  of  the relatively low  waste-
water  pH.   Also, increased ammonia oxidation capability would be provided  for
the  peak ammonia  loading time of  the year  (i.e.,   summer,  tourist  season).
Better  and possibly near  complete nitrification  may occur  under  existing
loading conditions using all  of  the  tower, except when  shock loading  condi-
tions  occur.   To  adequately handle the shock loads,  tower acclimation  using
chemical  ammonia  addition  may be  required.   Then,  as plant flow  rates  and
tower  ammonia  loadings  increase,  pH  adjustment may  be necessary to  increase
the rate  of ammonia  oxidation to  consistent  conversions of greater  than 90
percent.    It  is  noted  that  the  existing  nitrification facilities  are  not
required to perform  at high levels (i.e.  > .90 percent  ammonia oxidation  effi-
ciencies to meet the  original  projected design requirements.

DENITRIFICATION

    The UTSD plant was designed to oxidize ammonia  through the nitrification
tower.   Solids that  were generated and  sloughed from the tower were  to be
removed in  the mixed media filters.   This combination of  unit  processes  was
thought to have a  potential for nitrogen removal by denitrification within  the
mixed media filters.   If this  was  feasible, less expense would be encountered
because the filter could serve a  dual  purpose as a polishing filter and as a
support media  for  the denitrifying micro-organisms.   The  evaluation of  the
suitability of the mixed media filters for  full scale denitrification was com-
pleted during  two  time  periods.   Period  A lasted  for  34  days (4/3/78  to
5/9/78) and Period  B for 24  days (5/21/78  to  6/14/78).   Twelve  days time
separated the  two  periods.  The two time  periods were differentiated by  the
number of filters  on  line  and  by  a slightly different wastewater temperature.
During Period A, one  filter was on line and the average wastewater temperature
                                     91

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was 9.4°C.  During Period B,  two  filters  were operated and the average waste-
water temperature was  13.1°C.   Two filters were  placed into operation during
Period B because of an increase in the plant  flow rate, and because the filter
used in Period A had a tendency to plug when  methanol was added.

    Filter  influent and  effluent  flow proportioned  samples  were  collected
every two hours for  a  24-hour period from  Sunday through Thursday.   Analyses
conducted  on  most  of  the  composited  samples  include  N02/N03-N,  NH3-N,
TKN, ALK, COD, BOD5, and  TSS.  Temperature,  D.O.  and  pH tests were conducted
on grab samples.   The  performance of the filter  with  respect to run time and
backwash  requirements  was  also  of special  interest.    Therefore, filtration
rate, run time, head loss,  backwash rate and  backwash  duration  information was
collected prior to, during, and after the denitrification study.
Start-Up Interval

    Methanol was added  to  the  filter  influent  to  encourage  the  denitrification
process.  The methanol  storage and feed system to provide  this  capability  was
designed and installed  as  part of  the research project.   Methanol  was  added to
the  filter  influent at a  point preceeding  the existing in-line  mixer.    The
amount  of methanol  added  to  accomplish  denitrification  was  carefully con-
trolled,  since  it  was  assumed  that excessive  methanol addition would  lead to
"break-through"  and an increased BOD5 and COD  concentration  in the  filter
effluent.   The  theoretical formula  for  determining the  amount  of  methanol
required  has been  developed by McCarty, et.  al.  as  follows (3):

          Cm -  (2.47)  (N03-N) + 1.53  (N02-N)  +  0.87  (D.O)
              where:   Cm - mg/1 of methanol  required.
                       N03-N =  mg/1 of nitrate  nitrogen in influent.
                       N02~N =  mg/1 of nitrite  nitrogen in influent.
                       D.O. = mg/1  of  dissolved oxygen in influent.

     Assuming  that  typical  (4)  influent  concentrations  to a  denitrification
process would be  25 mg/1 nitrate,   0.5  mg/1   nitrite,  and 3  mg/1 D.O.,  the

                                       92

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 theoretical amount of methanol indicated by  this  equation to achieve complete
 nitrogen removal would be 2.5 times the amount of  nitrate in the feed system.
 Using the  above  assumed concentrations, the  methanol requirement  to satisfy
 the D.O. demand would be 4 percent of the total feed requirement.  The percen-
 tage of  methanol to  satisfy  the D.O.  demand for  the UTSD system  was  much
 greater  than 4 percent.   This  increased demand of methanol to satisfy the D.O.
 requirement greatly influenced the start-up procedures.

     The  combined average  of the results for  both Period  A  and Period B  are
 shown in Table 26.   Also shown is information collected prior  to the denitri-
 fication study.  The start-up interval  was  separated into  two time frames.
 One was  labeled "Methanol Less than D.O. Requirements" (i.e. less  than  0.87  x
 D.O.  concentration) and the other  "Methanol  Greater than  D.O.  Requirements".
 As  shown in  Table  26, N02/N03~N  removal  prior to  the denitrification  study
 did not  exist, in  fact  an  increase  occurred in  the N02/N03~N  concentration
 of  the filter effluent.    Correspondingly,  there  was an expected reduction in
 the NH^-N and alkalinity  concentrations  of the  filter effluent.   Apparently,
 sufficient  D.O. existed  in the  filter  influent to allow nitrification to  occur
 within the  filter.
    During start-up of  the denitrification  study, methanol was  initially added
in small  quantities which were gradually increased.   It  was felt that exces-
sive  methanol  additions  would lead to  breakthrough and  an increase  in the
BOD5  concentration of  the  final effluent.    Therefore,  during  the initial
start-up  period  the  amount of methanol  that  was added was  not sufficient to
reduce  the  D.O.  concentration to a point  where  denitrification would become
predominant.  An average  9.6 Kg/day (21.1 Ib/day) of methanol was added where-
as the  methanol  requirement  to  satisfy  the D.O. requirement was  16.8 kg/day
(37.1 Ib/day) (i.e., 0.87 x mass  of D.O.  in filter  influent).   The result was
that  sufficient  D.O. still  existed  to  allow  nitrification to  dominate  the
reaction  within  the  filter,  and  the  effluent N02/N03-N  concentration  at
6.5 mg/1 was greater than the influent concentration at 5.5 mg/1.  However, at
the same  time,  the effluent  BOD5 concentration  increased  by  about  100  per-
cent  to 16  mg/1,  indicating that  some  methanol breakthrough  occurred.    It

                                     93

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         TABLE 26.  SUMMARY OF DATA  COLLECTED DURING PERIOD A AND
              PERIOD B OF THE DENITRIFICATION SPECIAL STUDY
Start-Up (Acclimation)
Prior To Methanol Methanol
Evaluation Less Than Greater Than
Parameter Periods D.O. Required D.O. Required
Number of Days
(Combined Periods)
Wastewater Flow (mgd)
Methanol Added (Ib/day)
M/N Ratio (Ib/lb)
Methanol Demand for
Oxygen Req'd (Ib/day)*
D.O. Inf (mg/1)
N02N03-N Inf (mg/1)
Eff (mg/1)
Removal (%)
Filter Head Loss Rate
H/L (ft/hr)
Filter Rate (gpm/ft2)
BOD5 Inf (mg/1)
Eff (mg/1)
Removal (%)
TSS Inf (mg/1)
Eff (mg/1)
Removal (%)
COD Inf (mg/1)
Eff (mg/1)
Removal (%)
TKN-N Inf (mg/1)
Eff (mg/1)
Removal (%)
NH4-N Inf (mg/1)
Eff (mg/1)
Removal (%)
Alkalinity Inf (mg/1)
Eff (mg/1)
Removal (%)
Organic Nitrogen
Inf (mg/1)
Eff (mg/1)
Removal (%)

35
0.46
0
0

25.1
7.5
5.3
6.5
-23

0.26
2.22
24
8.1
66
12
4
64
45
34
24
13.7
11.4
17
10.6
9.2
13
74
63
12

3.1
2.2
29

11
0.69
21.1
0.67

37.1
7.4
5.5
6.5
-18

0.50
3.03
27
16
41
11
2
75
43
34
21
8.3
6.7
19
6.5
5.6
14
64
57
11

1.8
1.1
39

14
0.72
72.1
1.97

35.5
6.8
6.1
5.3
13

0.61
2.31
36
17
53
18
3
83
47
39
17
9.5
7.8
18
7.2
6.3
13
68
72
-6

2.3
1.5
35
Methanol
Full Feed
Interval

34
0.60
111
2.64

27.8
6.4
8.4
3.8
55

0.85
2.26
30
19
37
19
4
78
49
40
18
8.3
6.4
23
6.3
5.7
10
57
64
-12

2.0
0.7
65
 mgd x 3785 = cum/day; Ib/day x .454 = kg/day;  gpm/ft2 x 40.7 = 1/min/ sq
*Calculated assuming 0.87 Ib methanol per 1.0 Ib D. 0.
m
                                      94

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 should be noted that the methanol concentration in the filter effluent was not
 measured, thus it was  not known if the  increased BOD5 concentration  was due
 to methanol or due to  a  byproduct  of  the reaction.  The  term methanol break-
 through was used to  describe increased  organics  in the  efluent  whch contri-
 buted to a higher BOD 5  concentration.

     Despite the methanol breakthrough  it  was decided to add methanol at a rate
 that exceeded  the D.O.  requirement. When this was done,  denitrification began
 to dominate the reaction and the study was considered  to change from  a pre-
 start-up to a  start-up condition.   Period  A had  pre-start-up interval  of  9
 days and Period B only 2 days.   For  each start-up interval, 7-days  time was
 required before the  denitrification rate  reached its full potential.  The con-
 clusion was that the  true  start-up  condition  was reached only  after  the
 methanol feed   rate  exceeded the D.O. requirement,  and was  not heavily  in-
 fluenced by the pre-start-up time period  when the methanol  feed  rate  was less
 than the D.O. requirement.

     An  average N02/N03-N removal  of  13   percent  occurred  during the  start-
 up period when  the  methanol feed rate was greater than the  D.O.  requirement.
 Correspondingly,  the filter effluent  BOD 5  concentration  was greater  at  17
 mg/1  than during  the period prior  to  the study at 8.1  mg/1.   However,  con-
 clusive  evidence  of methanol breakthrough did not exist because  the  influent
 BOD5  concentration during start-up  at  36  mg/1 was  also  greater than prior  to
 the  study at 24 mg/1.   But, a trend  for a slight  increase in effluent  BOD5
 due  to methanol breakthrough is evident.

    The  influent  TSS concentration was"also  slightly greater during start-up
 at  18 mg/1 than prior  to  the study at 12 mg/1, but  the effluent TSS concen-
 tration was better during start-up  at  3.0 mg/1 than prior to the  study at 4.3
mg/1.   Better  TSS'removal  occurred indicating  that  biological growth within
 the media enhanced the  filtering action.   However, this biological growth  also
reduced  the filter run time and increased  the filter  head loss  rate which
eventually caused the study  to be halted.
                                      95

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Methanol Full-Feed Interval

    Methanol was initially added  to  the filters in small amounts to encourage
the growth  of the denitrifying  microorganisms and  to  minimize breakthrough.
The dosage  was then gradually  increased as denitrification  proceeded.   This
period of evaluation was called  the  methanol  full-feed interval.   The full-
feed  operating interval  of  Period A  was 19  days  and  for  Period B  15 days
(total of 34  days).   During  each of these full  feed  operating intervals the
amount of methanol added varied  which  provided different  methanol to nitrate
(M/N)  feed  ratios.    The ratios encountered  includes  the  requirements  for
nitrite and oxygen.  Typically, methanol  requirements for  these  parameters are
small relative to  the nitrate requirement (4).  In this report  the M/N  ratios
presented were calculated using  mg  of methanol  fed per  m g  of N02/N03-N in
the influent  as a  basis.   It is noted, however, that the methanol requirement
to satisfy  the oxygen demand was higher than typical.  Actual M/N ratios to
achieve complete  denitrification reportedly have ranged from 2.5 to 3.5  (4).
Similar ratios were  tested during the  UTSD denitrification study.  The percen-
tage  removal   of  N02/N03~N  compared  to the corresponding M/N  feed  ratio is
shown in Figure 18.  Data  to  make  this  analysis was  available  for twenty-one of
the thirty-four full feed days.

    The  average  N02/N03-N  removal   during  methanol  full-feed  was  55  per-
cent,  and  ranged from  29  percent  to  99 percent.    This range  of removal
appeared to be directly  related to variable M/N ratios  as  shown in  Figure 18.
A linear relationship  was  developed between the  N02/N03-N  removal percen-
tage  and the  M/N  feed  ratio.   The number of data points for  this  analysis  was
limited  due  to  the  relatively  short duration  of  each of  the study periods
caused by filter  plugging problems.   As  shown in Figure 18,  a  M/N feed ratio
of  about  4.4 is  indicated to  achieve 90  percent  removal  of  N02/N03-N,
which is higher  than the reported values mentioned earlier.   Several  reasons
may  have  contributed  to  the   higher  M/N  ratio,  including  relatively  low
operating  temperature, too  short a reactor detention  time,  and  a  relatively
high  influent D.O. concentration.
                                       96

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                                           •PERIOD A, TEMP = 9.4°C
                                                    DT=20MIN
                                          APERIOD B, TEMP = 13.1 C
                                                    DT = 26 MIN
                                    M/N  RATIO
    Figure 18.  Percent N02/N03-N removal versus methanol to nitrate feed
                ratio for Period A and Period  B  denitrification study.
    The average wastewater  temperature for Period A was 9.4°  C  and for Period
B 13.1° C.  A slight  trend  for higher  removal  at a given M/N ratio  when the
wastewater  is  of  a higher  temperature is qualitatively illustrated  in Figure
18.   More af  the  data points  for NC^/NOg-N removal  for  the higher  tempera-
ture Period B  are  above the line  of best  fit.   However,  significant  and con-
clusive data does not  exist with  these data points.
    The reactor  detention time varied from Period  A to Period B,  because one
filter was  used during  Period A and  two filters  were  used during Period  B.
The average wastewater  flow rate during  Period  A was 1820  cum/day (0.48  mgd)
and during  Period  B,  2840  cum/day  (0.75  mgd).    The  corresponding  reactor
detention times with the  appropriate  number of filters on line was 20  min for
Period A- and  26 min for  Period B.   Reactor detention  time was determined  by
using  the  entire  volume of  the mixed  media pressure  vessels.   Media  only
occuppied approximately one  half  of  the reactor  volume,  and therefore  only
about one half  the  detention time  calculated was under packed  bed  conditions.
                                      97

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These detention  times  were apparently sufficient to  allow  denitrification to
proceed, but  may have  been too  short  to  allow complete  denitrification in
accordance with available methanol.
    During the  periods of study  the average influent D.O.  concentration was
relatively high at 6.4  mg/1 and  the  N02/N03~N concentration  relatively low
at 8.4 mg/1.   The calculated M/N ratio includes the oxygen requirement because
it is  typically small (4 percent)  relative to the nitrate  requirements (4).
For  the full  methanol  feed period  shown  in Table  26  the  average  oxygen
requirement was 25 percent  of the  M/N  ratio.   If the  M/N ratio of  4.4 to
achieve  90 percent  N02/N03~N  removal,  as  indicted  in  Figure  18,  was  ad-
justed for the oxygen requirement, then the M/N ratio would  be  3.3 and move in
line with  reported values.   The large amount  of methanol required to satisfy
the  oxygen requirement  at   the  UTSD was  felt to  be  the major contributing
factor  to  the  higher than  expected M/N  ratios per  unit  NC^/NOg-N removal
shown in Figure  18.

    During full methanol feed  some methanol  breakthrough  apparently existed
because  both the  BOD 5  and  COD  concentration  of  the  filter  effluent were
greater than prior to  the study and  their respective removal efficiencies were
lower.   The  effluent BODj concentration  increased  from 8.1  mg/1  to  19 mg/1,
and  the 8005 removal  efficiency decreased  from 66 to  37   percent.   The ef-
fluent  COD concentration  increased from 34  mg/1  to  40 mg/1,  and  the COD
removal efficiency decreased from 24 to  18 percent.   It  should also be noted
that  most  of  this data  was collected  when  the  N02/N03~N   removal  was less
than  90 percent,  and methanol addition  was  apparently  less  than  the N02/~
   ~N requirement.
    The only other major  chemical change in the filter effluent that was mea-
sured during the denitrification  study  was  in  the alkalinity.  During methanol
addition the alkalinity of  the  filter effluent was  greater  than  the  filter  in-
fluent.   The TKN removal was  slightly  higher  and  NH3~N  removal was slightly
lower.  The overall  results of the  denitrification study to this point  indi-
cates   that  methanol  addition   to  the   mixed  media  filters  does   allow
                                      98

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denitrification  to proceed,  and 90  percent N02/N03~N  removal  can  occur  if
sufficient  methanol  is added  to  achieve  the  necessary  M/N  ratio.     Some
methanol  breakthrough occurs.,  but  does not  increase the  BODc  concentration
to unacceptably high  values.  However, as  shown in Table 26,  the  filter's  rate
of  headless  (H/L)  increased  significantly when  methanol  was  added.    This
increase  in the rate  of  headless  eventually caused the study to  be halted and
will be further discussed.

Filter Performance (Physical Parameters)

    The increase  in  the filter headless rate could  be  attributed to  an in-
crease in solids production  from denitrification  and/or  to the type of  solids
that were generated.    The theoretical  formula  for  solids  production  is  as
follows:

    Cb = 0.53 N03-N + 0.32 N02~N + 0.19 D.O.
         where Cb = biomass production - mg/1
                N03~N = Nitrate concentrations influent - mg/1
                N02~N = Nitrate concentrations influent - mg/1
                   D.O. = D.O. concentrations influent - mg/1

    Using  the full-feed  average N02/N03~N and  D.O.  concentrations at  8.4
mg/1 and  6.4  mg/1,  respectively, the theoretical  biomass  production  was cal-
culated at  5.7 mg/1.   This value was  30 percent of  the average  influent TSS
concentration of 19 mg/1.  This increase in the solids removal  requirement may
have caused the  filter  headless rate  to  increase somewhat,  but not  to  the
extent that occurred.

    The rate  of  filter headless  was  obtained by  dividing  the change  in the
filter loss of head between backwashes (H  in Hg  or ft of  H20) by the  length
of time between backwashes (L in hours).  Typically, the change in filter loss
of head  between backwashes  was  about  3.7  m  (12  ft).    The  parameter that
changed the H/L  ratio was  the  length of  time  between backwashes.  A low H/L
ratio was desirable because  it  indicated that  there were a minimum  number  of
filter backwashes required.
                                     99

-------
    The daily average  H/L ratios for both Period A  and Period B are  shown in
Figure  19.   The H/L  ratio during  the  methanol full-feed  interval is  shown.
The average  filtration rate  during these  periods  was  92.0  1/min/sq m  (2.26
gpm/ft2).
      —  6
      cc
      X
      x  4
      i
      ui
      a  3
      I  2
      o
                       PERIOD A
                                  PERIOD B
            •; i  i  i i  i	.I.	i—i—i—i—i  i_i—i—i—i—i—i—i—\—i—i—i—i—i—i—L_
          19  21  23 25 27  29  1  3   5   7   9   31  2   4    6   8  10  12  14
                 APRIL
                     MAY
                     1978
                                                     JUNE
                                                     6 -
                                                       cc
                                                       X
                                                     4 x
                                                       ui
                                                     3 I
                                                       V)
                                                     2 O
                                                                        111
    Figure 19.
Filter head loss rate during Period A and Period B methanol
full-feed operating interval,  (ft/hr  x 0.305 = m/hr).
    As  shown for Period A, the H/L ratio increased during the end of April and
 then  decreased again.  The reason for  this increase was  attributed to an in-
 creased wastewater flow rate.  In Period B,  the H/L ratio increased on 6/1/78
 and again on  6/10/78, and  decreased on  subsequent days.   In  both  of  these
 cases the filters were taken off line  for a period of up  to  24 hours,  which
 enabled them to recover somewhat.  However,  as  shown,  the H/L ratio increased
 significantly on  the last operating day  of both  periods.   Filter run  times
 were  reduced from about 24 hours to only 2 to 3 hours in both periods, and the
 system had to be shut down in both cases.   This substantial reduction in fil-
 tration capability was the single most  detrimental aspect concerning  denitri-
 fication using the mixed media filters.
                                       100

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    It  was  concluded from  these  results  that  substantially  lower  surface
loading rates would  be required if denitrification using a mixed media filter
is  to be  feasible.   However,  several  significant aspects concerning  the  UTSD
study  temper this  conclusion.   The  filter influent D.O.  concentration  was
higher  than  typically expected and  probably contributed to excess  biological
growth  on  the filter media.   The  type  of  biological growth and/or  the amount
of growth  associated  with  these higher D.O. values may have enhanced  the  fil-
ter plugging problem.   JFull documentation  as  to  the validity of co-currently
utilizing  mixed media  filters for  filtration  and  denitrification  cannot  be
made  based on  these  results.   What  can  be concluded  is that  the  dramatic
impact of  filter plugging  on this dual usage of mixed media filters certainly
makes  the denitrification aspect  certain  and worthy  of  special   attention
during similar  future  studies.  Furthermore, a  full-scale  system design should
not be completed without further  study.

    The filter  backwash rate and duration during the dentrification study  was
maintained  at  509  1/min/sq  m  (12.5  gpm/ft2)   and 15  min,  respectively.
Because of  the  relatively  short  periods  of  study, no  attempt was  made  to
change the backwash rate or  duration during each  evaluation period.  After  the
evaluation had  been  completed,  the backwash rate  and duration were  changed  to
determine  any  effects  associated with  the type  of  backwashing.    In  total,
three different types  of backwashing were  investigated.   The first  type was a
continuation of the  backwash  rate  of  12.5 gpm/ft2  and  duration of  15 min.
This was implemented after Period  A  on the one  filter that was used for deni-
trification  during  that period.   The  H/L  ratio initially was  about 6.0,  and
the backwashing frequency  had  been  reduced to two  hour intervals.    After 6
days and  12  backwashes, the H/L  ratio decreaed  to  0.5 and  the  backwashing
frequency had increased to 24 hours intervals.

    After the Period B evaluation, two different types of backwashing were  im-
plemented, one  on each of  the two filters  that were used for denitrification
during that  period.   On one filter  a  program of backwashing at a  lower rate
for a longer period  of time was  implemented.   A rate  of 8.7 gpm/ft2 for 23
                                     101

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min.   was used to  try to achieve  longer  scrubbing action  within the media.
The H/L  ratio initially was  about  4.5 and  the backwash  frequency  was about
every  2 1/2  hours.    After  seven  days  and  14  backwashes,  the  H/L ratio
decreased  to  0.5  and  frequency of   backwashing  had  increased  to  24  hour
intervals.    On  the other  filter  that  was used  for  denitrification during
Period  B, a  rate  of  13.2 gpm/ft2  for  15 min.  was used  to  achieve  a more
violent backwashing action.   In  this  case  the  H/L ratio was again 4.5  and  the
backwash  frequency was about every  2  1/2 hours.   After only 4 days and 8
backwashes, the H/L ratio  was reduced to 0.5 and the frequency of backwashing
had increased to 24 hour  intervals.  The higher backwashing rate  improved  the
recovery  rate of the filter and  represented a  better backwashing  program.
MIXED-MEDIA FILTRATION

     Effluent  from the  nitrification tower was  directed  to  the mixed-media
filters  where suspended  material was captured  and removed.   The  filtration
system consisted  of  four pressure vessels, each containing a mixture  of  three
different  types of media and a gravel support system.   The flow rate through
the  filters was matched to the nitrification tower  flow  rate  by the  use  of  a
bubbler-tube  system  and rate-of-flow  controllers.   Filter  backwashing  was
accomplished  manually,  but  could also be  initiated automatically.    Ozonated
plant  effluent served   as  the  backwash water  supply.    Backwash  wastewater
flowed to  a separate  storage basin and was eventually  discharged at  a control-
led  rate to the Thompson River Lift Station.

     Data  on  filter  performance was collected for  the period  of October,  1976
through  April,  1978.  Beginning in April,  1978,  a study  to determine the suit-
ability  of the filters  for  denitrification was  initiated.   Data during  this
period was included  in  the denitrification section  of this report.   A summary
of the filter's performance showing the mean values of  the data collected and
excluding  periods of excessive sloughing  from the  nitrification tower is pre-
sented  in Table  27.   The  effects of' sloughing  and other significant  events
that occurred during the evaluation period are discussed separately.   For the
periods  presented in Table  27, the overall  average wastewater  flow  rate was

                                       102

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       TABLE 27.  SUMMARY OF PERFORMANCE OF MIXED-MEDIA FILTRATION SYSTEM
        Parameter
Mean Value
Removal — %
BOD5-mg/l
    Influent
    Effluent
COD-mg/1
    Influent
    Effluent
TSS-mg/1
    Influent
    Effluent
Turbidity-NTU
    Influent
    Effluent
Ammonia—mg/1
    Influent
    Effluent
Total Phosphorus-mg/1
  35
  10

  56
  36

  22
   6
   6.1
   2.1

   5.9
   5.3
    71
    36
    73
    66
    10
Influent
Effluent
Fecal Coliform-#/100 ml*
Influent
Effluent
Flow — mgd
Range (1 Filter)
Range (2 Filters)
Hydraulic Loading-gpm/f t2
Range (1 Filter)
Range (2 Filters)
Head Loss Rate-ft/hr
Range (1 Filter)
Range (2 Filters)
Backwash Frequency-#/week
Range (1 Filter)
Range (2 Filters) .. ,;:
Backwash Rate-gpm/ft2
Backwash Time— min
Backwash Volume-gal
4.7
4.4
4.75 x 104
4.28 x 104
0.47
0.18 - 1.12
0.45 - 1.12
2.02
0.87 - 5.40
1.09 - 2.70
0.56
0.009 - 1.31
0.51 - 4.63
9.7
2-31
. 9 -; 46
13.0
14.4
26,096

6
10
	
	
	
—
	
	
    *Expressed As Geometric Mean
    mgd x 3785 = cu m/day; gpm/ft2 x 40.7 = 1/min/sq m; ft/hr x 0.3048 =
    m/hr; gal x 3.785 = 1
                                     103

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1780 cu m/day (0.47 mgd).   The  lowest flows received at  the  plant typically
occurred  during the  fall,  winter  and spring.    The  highest  flows  occurred
during  the summer  when  peak daily  flows  of  3785  cum/day  (1.0 mgd)  were
received.   During  the low flow  periods,  only one of the  four  filters  was in
service.  For approximately  three  months  during the summer, when the influent
flow was  typically greater  than 2840 cu m/day (0.75  mgd), two  filters were
utilized.   This approach  to filter  usage resulted  in  an  average hydraulic
loading of 82 1/min/sq m (2.02 gpm/ft2).

     The filter backwashing and  operating sequence utilized the following pro-
cedure:   a  predetermined maximum  filter head-loss  (i.e. 3.7 m  (12  ft)  of
HoO) was  set  on the  filter  control  panel,  and as the head  loss  reached this
level an alarm  was  sounded.   The operator then took  that  filter  off-line for
backwashing, and the  next filter in the series  was placed  in service.   In this
manner all four filters  were maintained  in an operable condition and were not
allowed to  be idle along enough to  become septic.  The  filter plugging rate
was quantitatively  measured  in  terms of the  head-loss  rate.   The head-loss
rate (H/L) was  determined by  dividing the head-loss  (H)  by the length  of time
between backwashes  (L).   The average  head-loss rate was  0.17 m/hr  (0.56 ft/hr
and varied  between  0.06  and 0.21 m/hr (0.2 and  0.7 ft/hr).   The  frequency of
filter  backwashing  averaged  about  ten times  per  week.    This  evaluation ex-
cludes  periods where excessive sloughing  of  solids  from  the nitrification
tower occurred.   When the towers were not  sloughing,  the influent wastewater
was  typically  of  high  quality  which explains the relatively  low head-loss
rates and long  filter runs.

     An average backwash rate of 530 1/min/sq m  (13 gpm/ft2)  for about 14.5
minutes resulted in the  utilization of 100 cu m (26,100 gallons) per backwash.
Backwash rates  were varied  throughout the evaluation period, but no evaluation
to optimize rates and minimize backwash volume was completed.

     In general,  the  filters worked  well in  polishing the  effluent  from the
nitrification towers  (influent  to the filter).   An  average 71 percent  reduc-
tion  occurred  in  BOD5, while  the  average  reduction  in  COD   averaged  37

                                      104

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 percent.  A mean  reduction of 73 percent for TSS and 66  percent  for  turbidity
 was  also  achieved.  Minimal  reductions  occurred in ammonia,  total  phosphorus
 and  fecal coliform concentrations.

     The  trends  in filter performance are  depicted graphically by the  weekly
 average values for  influent  and effluent  BOD5 and  TSS concentrations  shown
 in Figures  20  and 21,  respectively.   For the first five months of the  evalua-
 tion (i.e.  through  March,  1977)   consistent  BOD5  and  TSS removals  were
 achieved through  the filters  with concentrations in the  filter effluent aver-
 aging 5 mg/1  and  4 mg/1, respectively.  During  this  period one filter  was  in
 service   and   the   hydraulic  loading  was   approximately   70   1/min/sq  m
 (1.7 gpm/ft^).    For  the next  two  months  until a portion of the  plant was
 bypassed  for  modification in  June,  some  deterioration in  effluent  quality
 occurred.   The mean TSS  concentration in the  effluent increased to 7 mg/1, and
 the  BODc;  level increased  to  11 mg/1.   During  this time only one filter was
 in  service,   yet  plant  flow  had  increased significantly.    The  hydraulic
 loading to  the mixed media filter was  increased by about  60  percent,   to 110
 1/min/sq m  (2.7 gpm/ft2).   This higher  hydraulic  loading was  felt  to   be the
major factor that  contributed to the slightly deteriorated  effluent quality.
     The activated sludge  aeration  basins  were bypassed for two weeks in June
1977,  to  modify the gate  separating the  activated  sludge basins.   When  the
plant  was  placed  back in  operation  in  July,  two filters were  put  on line  to
handle the high summer flows.   With the two filters in service, the  hydraulic
loading still  averaged 102 1/min/sq m (2.5 gpm/ft2)  for the  months of July
and August, 1977.  However,  the filter influent TSS  and  BOD5  concentrations
increased to 38 mg/1 and 118 mg/1, respectively, which were the highest levels
reached during the total evaluation period.  Much of  the  BOD5  was in soluble
form which was a  result  of trying, to "start-up"  the  activated sludge process
during the high summer flow period.   It should also be noted that during this
time a higher than normal  strength  sewage  was  being received at the  plant  due
to contributions  of  waste from the dump  station,  including septic  tank  and
chemical toilet waste.   The  filters performed well in removing the  suspended
solids; however,  the  backwash frequency increased to  a high of  46  times  per

                                     105

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      O»N»D»J«F»M«A»M«J«J«A»S»O«N»D«J»F«M«A
 Figure 20.   Mixed media filter influent and effluent BOD^ concentration

             during the research project.
O)


(O
w
I-
 Figure 21.   Mixed media filter influent and effluent TSS concentration.
                                   106

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 week which  was  considerably greater  than the average  frequency of  10.   The
 BOD5 removal was not nearly as good as the TSS removal.

      Also during the summer of 1977, sloughing of the biological mass from the
 nitrification tower media  (plastic media was in  service)  occurred in quanti-
 ties that resulted  in almost  immediate  plugging of  the filters.   Typically
 when a period of sloughing  occurred the  biological mass from  the  tower would
 plug a filter within  10 minutes  and  another filter would  have to be  put  on
 line.    These extremely  low filter run  times  required frequent  backwashing
 which depleted  the  volume  of  backwash water.   When all of the filters  were
 plugged or when the volume  of  backwash water was depleted,  the nitrification
 and filtration systems were bypassed.   A change in  tower operation to provide
 for a more constant hydraulic  loading allowed the sloughing  problem to  become
 less severe, but the problem was  not  eliminated.   It was concluded that  with
 the occurrence of tower  sloughing,  the filters could  not  be depended  on for
 solids  removal.   This  conclusion  is significant when considering a design for
 a  solids  capturing process  following an attached growth nitrification system.
 It  is noted  that  a similar  plugging  problem occurred  with  the filters  when
 activated sludge solids were lost  from the  final  clarifier.   An overall  con-
 clusion was  that the mixed  media  filters  worked  very well to  polish the  normal
 effluent  of  the upstream processes, but  was not suitable  during   periods  of
 process upset  or tower  sloughing.   A sedimentation basin may  be  more effective
 during  periods of  upset such as sludge bulking  or  solids sloughing.  To  this
 end, a  possible  design  consideration for  the  UTSD facility would be to combine
 the  function of  the  tower wet-well with that of an  overflow clarifier.    With
 this option  available  the heavy solids could be removed by a sludge collector
mechanism, thus  eliminating  the filter's rapid plugging  problem.

     From September  1977, until  the end of  November  1977,  the  TSS and  BOD5
 concentration  of the influent  to  the  filters averaged  33  mg/1  and 32 mg/1,
respectively,  which  were lower than the  summer  loadings.  Respective concen-
 trations  in  the effluent were to 9 mg/1 and  12  mg/1.   The  mean hydraulic
loading  also  decreased  to  65 1/min/sq  m  (1.6  gpm/ft2).     The  decreased
loading allowed  the frequency of backwashing  to  return to more   reasonable
values, averaging once per day.

                                     107

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     From  December,   1977,  until  April,  1978,  consistent  TSS removal  was
achieved across the filter.  The mean TSS concentration in  the effluent during
this period was 4 mg/1.   BOD5 values in the  effluent  were more sporadic, but
the mean concentration was still  only  6 mg/1.   At the  same  time  the lowest
average head  loss rate  was achieved during  the  project at 0.07  m/hr (0.22
ft/hr).  This value is approximately half  of  the rate that existed during the
previous winter of 1977.  As noted by the TSS graph in Figure 21, the  influent
solids concentrations and effluent quality were  almost identical for these two
winter periods.  The  major  difference between the  1978 and 1977 winter filter
head-loss rate was associated with the  operation of the  activated  sludge  sys-
tem.  As previously discussed,  a higher mass  was held in  the activated sludge
system during  the  1978 winter, which resulted  in improved BOD5 removal.   The
sludge characteristics associated  with  the two  levels  of  activated  sludge  sys-
tem mass apparently were responsible for different forms  of effluent suspended
solids, and consequently different head-loss  rates through the  filters.

     In conclusion, the  mixed media  filters normally worked well to polish the
UTSD  plant effluent.    However,  during periods  of heavy  sloughing   from  the
nitrification  tower or periods of solids loss from the activated sludge clari-
fier bypassing of  the filters was required.
                                       108

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 OZONE  DISINFECTION

 General

     The  ozone disinfection  system  was not run  continuously during the  two-
 year  data collection  phase of  the  research project,  because several  system
 modifications  were necessary  before safe, continuous  operation could  occur.
 The  system was operational  on a periodic  basis,  and  during  portions  of  the
 two-year  data  collection  phase of the  research  project  separate  special
 studies were completed  to  evaluate the  performance,  design  and cost  aspects  of
 the system's operation.   This section,  of  the  report describes the  results  of
 the special studies.

     Data  collection for  the  ozone  system special  studies included chemical
 and microbiological analyses, ozone in air concentrations  and mass measure-
 ments, ozone in water-concentration  measurements, electrical  power consumption
 measurements and other miscellaneous measurements.   Since the use of ozone  in
 wastewater treatment is a  relatively new application, the equipment  and  proce-
 dures used to collect the  ozone  data are described.

 Data Collection

 Ozone in Air - Concentration and Mass Measurements—
     The  ozone  concentration  in the ozone/air  flow from  the generators was
measured by a wet  chemistry procedure  and  by  a  high concentration  continuous
 reading ozone  meter (Dasibi High  Concentration  Ozone  Meter,  Model   1003-AH).
 The wet chemistry method involved a  sodium  thiosulfate  titration of  a prepared
 solution of potassium iodide  which had  been exposed to a known volume  of the
 ozone/air flow stream.  A detailed description of the testing  and data record-
 ing procedures is included in Appendix  G.
     An alternate  acceptable  method of monitoring ozone  concentration  in air
was available  after the  Dasibi continuous  reading  ozone meter  was properly
set-up and calibrated.  Originally, meter  readings did not correlate with wet
                                      109

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chemistry results.   The problem was isolated  to  the ozone/air  and  purge air
flow rate to the meter.  Lowering  and  controlling the ozone/air and purge air
flow rates to about  2  1/min  resulted  in consistant meter readings that corre-
lated well with wet  chemistry results.  A comparison of meter results with wet
chemistry  results  is  shown  in  Table  28  and  Figure 22.   Due to  the  good
correlation between  wet chemistry and Dasibi  meter  results,  it was concluded
that  the  Dasibi  meter   could   be   used   to  determine  the  ozone  in  air
concentrations  so   that   additional  data  points  could  be   less  tediously
obtained.  However,  the Dasibi meter  was used to  obtain only about 25 percent
of  the  ozone/air  concentration measurements  used in  this report, because the
problem with the meter  was not  corrected until the later part  of the research
evaluation.
   TABLE 28.   SUMMARY  OF  COMPARISON  OF  CONTINUOUS  MEASUREMENT  DASIBI  OZONE
               METER RESULTS WITH WET CHEMISTRY  RESULTS	
   Date
                                7/19/78
                                                  7/21/78
                    7/25/78
Dasibi Meter
   Span Setting
Number of  Tests
Average  Wet Chemistry*
   Result (ppm(vol))
Average  Actual Dasibi*
   Reading  (ppm(vol))
Average  Difference (%)**
Range of Difference (%)
                                 80570
                                     4

                                  5598

                                  5532
                                  0.1
                              -0.2 to 2.0
   80570
       9

    5372

    5351
    0.4
-0.7 to 2.6
   80570
       5

    3222

    3204
    0.6
-0.7 to 1.7
  *Corrected to standard conditions of 1 atmosphere pressure and 25°C temp.
                        (Wet Chemistry - Actual Dasibi) (100)
                                    (Wet Chemistry)
**Percent Difference
                                       110

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     The   ozone/air  concentration   was
combined with  the  generator air flow to
obtain the mass  of ozone produced.   The
generator  air  flow was  measured with  a
Fischer   and   Porter   Series   10A3500
"Flowrator"  meter.   The  recorded  flow
was  corrected  to  standard  pressure  and
temperature conditions of one atmosphere
and 25°C.
S 600O
o.
a.
^5000
z
5
< 4000
111
1C
OC 300O
111
1-
UJ
S 2000
m
Q






/
DIRECT COR
o ACTUAL




/




/




/



RELAT

X



>•
ON
X





X






                                                0   1000 20OO 30OO 40OO 50OO 6000 7000
                                                  WET CHEMISTRY RESULT- PPM IVOL)
                                             Figure 22.  Comparison of  Dasibi
                                             meter and wet chemistry ozone/
                                             air concentration measurements.
      The ozone/air concentration  of the
 contact basin off—gas was measured using
 a  wet chemistry  procedure.   A detailed
 description  of  the   testing  and  data
 recording  procedures  'is   included  in
 Appendix H.   The flow  rate of  off-gas
 through the vent  duct was measured using a pitot tube.  The pitot tube was not
 ozone  resistant so the  off-gas flow  rate determinations  were made  with the
 ozone generator shut  down and only the air pretreatment  system running.   Off-
 gas  flow measurements  were  taken  at  different  air  flow  rates  from  the air
 pretreatment  unit.   The  data points were very reproducible  and a  curve was
 developed  relating   off-gas  flow  rate   to  air  flow  rate  from  the  ozone
 generation  system.   The curve was  used  to determine off-gas  flow  rate during
 testing  of  the  ozone  disinfection  system.   (See Table H-2 of Appendix H).  The
 off-gas  flow rate,  corrected  to  standard conditions,  was  coupled with the
 off-gas  concentration and was used  to  obtain the mass  of ozone contained  in
 the contact basin  off-gas.

 Ozone In Water  - Concentration Measurements—
     Ozone  residual   concentrations in  the  effluent  from  the  ozone  contact
basin were  initially  made using a volumetric titration procedure.   Using this
procedure it became apparent that  the color change at the end of  the titration
was nearly  impossible to  detect.    It was  decided that an  amperometric titra-
tion method would be  employed.  An  amperometric  titrator  was purchased and was
used  to  obtain ozone/water  concentrations.   During  the research  evaluation
                                      111

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period, good  disinfection results were  often obtained with  no  detectable or
negligible ozone residuals.

Electrical Power Consumption Measurements—
     Ozone generator and  air  pretreatment  power consumption measurements were
made with a Sangamo  type  S3DS watt-hour meter, which  was  tied into the elec-
trical feed lines to both the ozone generator and air  pretreatment  units.  The
meter  provided  the  capability to determine  totalized kilowatt-hour readings,
maximum kilowatt  demand readings and  instantaneous  kilowatt demand readings.
A sample of the data sheet used  to record  test  information  and calculate power
requirement values is included in Table G-2  of  Appendix G.

Miscellaneous Measurements—
     Other measurements and gauge readings were taken  in conjunction with gen-
erator production determinations as shown  in Table G-2. of Appendix  G.   The air
pretreatment  dew point was  measured  with a Shaw  Model "S"  Mini Hygrometer
which  had  a Red Spot probe.   Using the meter, the changes  in  air dew point
from the  air  pretreatment system were recorded throughout  the  day.    The air
dew point as measured by  this procedure typically ranged from -70°C to -54°C.
(Note:  new information developed in March,  1979  indicated  that  these  results
were inaccurate.   The  magnitude and impact  of  the  inaccurate readings on the
results are presented at  the  end of this section.

     The  air  compressor  seal water pressure reading was  recorded daily and
also every time ozone  generator production testing was  conducted.   The  seal
water  pressure  was  the  line  pressure  of the water that entered  the water,  ring
seal.   The pressure gauge was  located before a filter screen in the water
supply line.    When the  in-line filter screen became  plugged, varying  seal
water  pressure  indicated the varying  water  flowrate  to  the seal.  A  variable
flowrate  affected the compressed air  temperature, which  in  turn  affected  power
consumption of  the  refrigerant drier.
                                      112

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Data Evaluation and Discussion

     The discussion of  results from the research evaluation of  the UTSD ozone
disinfection  system is  separated into four general categories:   ozone  genera-
tion,  ozone system power requirements,  ozone  contacting system  and  disinfec-
tion performance.

     During the  UTSD research evaluation  the  ozone  disinfection system  was
intermittently operated.   Intermittent operation resulted from  numerous  prob-
lems  requiring  design  or  operations  changes.    Several  of  the  problems
encountered were associated with the "state of  the art"  design of one  of  the
first  full-scale ozone  wastewater disinfection  systems  in the United  States.
Much  conflicting  and  confusing  information  was  provided by  various   "ozone
experts" in regard to  the  UTSD  ozone  disinfection system.   The conflicting
information provided often  delayed the correction of the  design  and Operation-
al problems encountered.  The  major  disadvantage of the  intermittent  operation
of the ozone  disinfection system was  that  a  thorough  evaluation  of  disinfec-
tion performance was not achieved.

Ozone Air Pretreatment—
     The three components of  the ozone generation system were air  pretreat-
ment, ozone generator and power supply.  These three areas were  evaluated both
separately  and in combination  during the course of the  research effort.   The
ozone generation system performance was dependent upon  good  quality dry air.
As such, the operation and performance of the air pretreatment system was just
as important as the operation  and performance of the generator itself.

     Several  problems were  encountered  with  the air  pretreatment system  and
the potential for some  problems  to  reoccur exists.  Steps  are  being taken to
eliminate this potential.
     The air compressor for each  air  pretreatment  system was a constant speed
unit and continuously  discharged an  air  flow of  160  cu m/hr (94  scfm).   By
bleeding-off excess air, the air pretreatment system could operate at variable

                                      113

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air flow rates.  Originally, excess air from  the compressor was bled-off after
passing  through the  air drying  tower.    Each drying  tower was  rated  at a
maximum  air  flow  of  only  130  cu  m/hr  (78  scfm),  thus  was  constantly
overloaded.   This  caused an  excessive high dew point  of the  "dried" air.
Subsequently, a minor modification was  made by installing  a  bleed-off valve
after the  air  compressor and before  the  air drying tower  so  that excess  air
was bled-off before the  air  drying  tower.   Varible air flow not to exceed  the
air pretreatment system's ability to  provide dry air is highly desirable,  but
a more economical means  of providing  variable air  flow  is required.

     Compressed air was  directed  through a refrigerant  drier that  had  an input
voltage  of 440 volts.   This voltage  was  compatible with  the  voltage to  the
ozone  generator, but when  operational  problems  were  encountered  with  the
refrigerant drier it  was quickly  learned that all  parts locally available were
for 220  volt refrigeration  units.  These  parts were not  suitable for  the  in-
stalled  440 volt refrigerant drier,  and parts had to be special ordered which
delayed  the unit's repair.   The  time  delay for repair  of  the refrigerant drier
was the  main  reason  Generation  System No. 1 was  not  operable  during most  of
the time the production  data used for this report was developed.  To  maintain
both ozone generation systems fully  operational,  the UTSD will  have  to pur-
chase additional spare parts for  the  refrigerant driers.  Also, the UTSD staff
was not trained nor  had the  necessary equipment to  repair  the refrigerant
unit.   The corrective maintenance and spare parts  problems encountered with
the UTSD 440 volt  refrigeration system should be  considered during the design
of air pretreatment capability  for  other  ozone systems.

     Each  of the two  air drying  towers contained  activated alumina, molecular
sieves and alumina balls desiccant  material to absorb  the water in the air  and
lower the  dew  point to less than -51°C.   One tower  "dried" air from  the com-
pressor  while the other  tower was regenerated by  a  combination of heating  the
desiccant  material  to release the  bound water  and purging the tower  contents
with dry air to remove the  excess moisture.  The  towers were cycled for drying
and regeneration at 8-hour  intervals.
                                       114

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     Generally,  the air  drying towers  worked well  after  the  air  bleed-off
valve was moved  to a location  in  the air flow scheme  which was prior  to  air
entering the towers.  However,  "sticking" occurred  in the  linkage  of  the pneu-
matically operated  switching  mechanisms  used to alternate the towers  from  the
drying to regeneration  cycles.   The linkage was lubricated, but the  potential
for this problem  to reoccur still  exists.   The signal  for cycling the  drying
towers is  electrical while the tower switching  mechanism is  pneumatic.   If
problems are encountered  with the  pneumatic switching mechanism, the  electri-
cal system will  still  indicate that  the  towers are functioning normally even
though "wet" air could  be  passing  through the tower that  is regenerating.   If
this occurrs,  excessive moisture  could be  directed to  the ozone generator.
Under this condition the ozone  generator could be "flooded".  The  term flooded
is  used  to describe moisture  build—up  in  the  ozone  generator  which  causes
short-circuiting and can cause  electrode tube and/or fuse  failure.

     On several  occasions flooding  of  the  ozone  generator did occur.   Once
flooding occurred  due  to  a problem  with  the refrigerant  drier.   The  refrig-
erant drier motor overheated  and burned out, for  an as  yet unknown reason.   A
new refrigerant  drier  was ordered.   When  received, careful electrical  checks
were made during its installation  to  try to  isolate the problem.
     Flooding of the ozone  generator  on three other occasions has been  tenta-
tively associated with  problems of variable  seal  water  pressure to the  water
ring air compressor.  These generator floodings were expensive because several
electrode tubes and fuses blew out.   The greater  the  seal water pressure  the
greater the water flow  rate  through  the compressor and the lower the tempera-
ture of compressor air.   The temperature of  the  compressed air was important
because if the temperature  was too high  the  refrigerant  drier could not cool
the air to reduce the dew point  and  the air drying tower was overloaded.   The
flooding problems were believed  to have  occurred due to plugging of  an in-line
filter screen which was  used to remove  any  particulate  matter from the  water
that was directed to the compressor.  Plugging caused  the  flow of water  to  the
compressor to decrease  and  the  temperature of the compressed air to increase
and eventually led to overloading  of  the drying  tower.  The entire  seal  water
                                      115

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supply system  is  being re-evaluated to determine  what  design modification or
preventive maintenance checks can be instituted to reduce the frequency and/or
effects of the screen plugging problem.

     Although sources of ozone generator flooding  problems have been isolated,
the potential  of  flooding  still  exists.    It appears  that  a high  dew point
alarm and  an  associated automatic generator  shut^off  is  necessary to prevent
the expense and loss of production associated with generator flooding.  Origi-
nally, the relative air dew point  was  monitored with cobaltous chloride color
changing indicator.   This  indicator was inadequate  as  an alarm or protection
device for the ozone generator for  two reasons:   1)  Someone had  to  see the
color change  and shut  down the  system before  flooding  occurred and  2)  the
color change was  not sensitive to gradual  changes in  dew  point  so potential
problems could not be detected until they were quite far  along.

     A dew point  indicator was purchased as  part of  the research project to
obtain more  exact information on  air  dew  point  versus generator production.
This indicator has greatly  aided  in  the detection of changes in dew point and
correction of  problems before flooding of  the  generator occurred.   However,
the potential  for generator flooding still  exists since  operator observations
of the indicator  on  a continuous  basis is  still  required to detect any prob-
lems.  As a better solution, a high  level dew point  alarm and associated auto-
matic generator shut-down  is being considered.   To date,  this would have saved
the UTSD at  least  $1,600  in  electrode tubes and fuses during  the  past two
years of operation.

Ozone Generator Production—
     Many  parameters can  influence  the rate of  ozone production including:
power supply,  air dew point, ozonated  air  temperature which is influenced by
the volume of  air directed through the  generator  and the  ozonated air heat re-
moval capability  of  the cooling water  jacket.  These items are not all  inclu-
sive,  but were  selected  for  analysis because  they  represented  those items
within the realm  of  operational control for the  UTSD system.
                                      116

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      The UTSD ozone generators were designed to supply ozone at a rate of 34.3
 kg/day (76  Ib/day)  at an air flow of 118 cu m/hr (70 scfm).  The ozone produc-
 tion for Generation System No. 2 only is discussed, because Unit No. 1 was not
 operational.   The production rate  for  different air dew  point  levels  will be
 presented because the ozone production rate decreased as  the  dew point of the
 air  increased.   This change  in  production may  be a significant  operational
 consideration with respect to continuous,  satisfactory  effluent disinfection.
 The  production rate will also be compared to the relative power setting of the
 generator for two different air flow rates, namely the design air flow rate of
 118  cu m/hr (70 scfm) and a lower air flow rate of 79 cu m/hr (47 scfm).

      The air  dew point readings increased  proportionately to  the drying tower
 operating time.  Typically,  soon after a  regenerated  tower came  on-line and
 began drying,  the air dew point reached its lowest level.   As  the  tower dried
 more  air, the dew point increased.  Apparently, as the  desiccant absorbed and
 contained more and  more moisture,  less  moisture was absorbed as  indicated by
 the dew  point readings.   The  rate of increase of the dew  point  was  greater at
 the design  air flow rate of 118 cu m/hr  (70  scfm)  than  at the  lower air  flow
 rate  of  79  cu m/hr (47  scfm).   The changes in  air  dew  point for the  two air
 flow  rates  versus drying tower  operating  time  is shown in Figure 23.
     The  drying time per operating  cycle
for each  tower  was eight (8) hours.   The
lowest dew  point  reading shown in  Figure
23 is -72°C., although readings as  low as
-74°C  were achieved.    The  highest  dew
point recorded  was -54°C.   All dew  point
levels recorded,  except  when obvious  air
pretreatment problems were noted  to  cause
generator floodings, were better  than  the
manufacturer's  rated minimum dew   point
level of  -51°C.   The UTSD ozone air pre-
treatment  system   functioned  very satis-
factorily.
              0:47 SCFM AIR FLOW
              A =70 SCFM AIB FLOW
   01   2345678
   DRYING TOWER OPERATING TIME-MRS.
Figure 23.  Change in air pre-
treatment dew point with drying
tower operating time (scfm x
1.70 = cu m/hr.)
                                      117

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     The  change in  ozone  production per
degree of  change in dew  point  was evalu-
ated  at  different  generator   power  set-
tings.  Two  power  settings were evaluated
and results  are  shown  in  Figure 24 and in
Table 29.   In general, the ozone produc-
tion level decreased as the air dew  point
increased, even  though the manufacturer's
rated dew point level  of -51°C as measured
by  the  dew  point  indicator was achieved
throughout the drying  cycle.

     As  shown   in  Table  29,   the  mass
decrease  in ozone production  per degree   Figure 24.   Change in ozone pro-
change in  dew point  was  about  three  times   duction with dew point at two
                                             generator power settings (Ib/day
greater for  the  130  amp power setting than   x Q.454 = kg/day).
for  the  40  amp  setting.   However, the
percentage change was  slightly  less  for  the 130 amp setting at 1.70%/°C. than
for the 40 amp setting of  1.93%/°C.   From the data  presented it was  shown that
OZONE PRODUCTION - LB/DAY
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              AIR DEW POINT -°C
    TABLE 29.  EFFECT OF DEW POINT AND POWER SETTING ON OZONE PRODUCTION
                   Dew Point
130 Ampere
 40 Ampere
Maximum Production - 72°C.
                   - 70°C.
Minimum Production - 56.5°C.
                   - 59.5°C.
Total Dew Point Increase
Ozone Production Decrease
Specific Ozone Production Decrease
     Mass Decrease
     Percent Decrease
 57 Ib/day

 42 Ib/day

 15.5°C.
 15 Ib/day


 0.97 lb/day/°C.
17.1 Ib/day

13.6 Ib/day
10.5°C.
3.5 Ib/day


0.33 Ib/day/°C.
Ib/day x 0.454 = kg/day
                                      118

-------
 ozone  production  decreased  considerably with a decrease in dew point,  which is
 important with  respect  to ozone  dosage  to  the wastewater.   The implications of
 these  findings  on design and  operation  are significant.

     At  the UTSD  plant  the  wastewater flow rate was controlled  through  a  flow
 equalization  basin and a negligible variation in  daily plant  flow occurred.
 The  ozone dosage  to  the effluent  was  manually  controlled  by  adjusting  the
 generator power setting.   However,  at  a given power setting  the ozone  dosage
 decreased as  the  dew  point  increased.   The potential magnitude of  the  decrease
 in  ozone dosage  for  observed  changes in  air  dew point  is  summarized  in
 Table  30.
    TABLE 30.  POTENTIAL DECREASE  IN OZONE DOSAGE  FOR  OBSERVED  CHANGES  IN
               AIR DEW POINT  (CONSTANT GENERATOR POWER SETTING  AT  130 AMPS)
                               Air Dew Point*
                                    -72°C.
                         Air Dew Point
                              -56.5°C.
Wastewater Flow (mgd)
Ozone Dosage
     (mg/1)
     (Ib/day)
1.37
5.0
57**
1.37
3.7
42**
    mgd x 3785 = cu m/day; Ib/day x 0.0189 = kg/hr.
   *The manufacturer's minimum rated dew point level was -51°C.
     As shown in Table 30, the ozone dosage could vary from 5.0 to 3.7 mg/1 if
the air  dew point  changed from -72  to -56.5°C  (a. change that  was observed
during a  typical  drying cycle).  A change in dosage because  of  dew point is
important from  a  design and operation  basis  because disinfection performance
is  influenced  by ozone  dosage.   Therefore,  ozone  production information at
different power settings  and  at variable  dew point  levels   are  required in
order to properly design and operate ozone disinfection systems.  In the final
analysis it may be required that ozone  systems be designed with multiple units
which have  the  air  pretreatment drying towers changed sequentially  so  as to
reduce the overall effect  of a rise in  dew point on ozone production.
                                     119

-------
     It should be noted  that  the sensitivity of the system disinfection capa-
bility to ozone dosage was  not  evaluated due to the intermittent operation of
the UTSD  ozone  system.   It may be that  an ozone dosage between  3.7 and 5.0
mg/1 yields  the same  general  disinfection level, especially when other system
variables like  effluent COD, TSS  and fecal  coliform  concentrations are con-
sidered.  If the disinfection capability  is  not  overly  sensitive to  this range
of dosages the dosage variation because of  dew point would not be as  critical.
This aspect  should be further evaluated.   However, it  is still concluded that
more  information  should   be   developed  by  ozone  manufacturers   on  ozone
production versus dew point levels and ozone production versus generator power
settings  in order  to provide  design engineers and  plant  operators  with a
better basis for ozone system design  and  operation.

     The major factors affecting ozone production  are  generator power setting,
air dew point and ozonated air temperature, which is influenced  by the air
flow rate to the ozone  generator and the heat removal  capability of  the cool-
ing water  jacket.   The  cooler  the temperature   of  the  ozonated  air, the less
rapid ozone  will be decomposed  after  it  is generated.  The UTSD ozone  genera-
tor begins producing ozone  at a consistant,  reproducible  level at a  power set-
ting  of 40  amps.   The maximum power setting tested  was 150 amps, when  the
generator voltage  was 450 volts.   For  the  production  evaluation  the mass of
ozone produced was  determined  for power  settings  at  10 amp intervals  between
40 and  150.  The ozone  production values shown  in this report were  taken when
the air dew  point was between -70°C.  and  -74°C as  indicated  on the  Shaw meter.
This dew point level represented the  best condition for ozone production with-
in the  limits of the air pretreatment unit.

     To insure that  the cooling water system was  performing at optimum condi-
tions,  the cooling water jacket was  inspected for  possible  scaling  which could
have reduced its heat  removal  effectiveness.  No  scaling was noted  at  cooling
water jacket sites that  were inspected.   This was  as  expected because no scal-
ing problems were encountered  on  other  equipment in  the  plant  that used  the
same water  supply.   The temperature  of  the cooling water ranged between  10°C
and 12°C, which was within  the  ozone  manufacturer's specifications.
                                      120

-------
     The actual  temperature of the ozonated  air was not  recorded.   However,
the  relative temperature  of  the  ozonated  air was  investigated within the
limits of  the UTSD system  by adjusting the  air flow rate  to  the generator.
The design air flow rate of 118. cu m/hr  (70  scfm)  was expected to develop the
lowest ozonated air temperature, and in turn produce  the highest mass of  ozone
at a given power setting.  The lower air flow rate of 79 cu m/hr (47 scfm) was
expected to  produce a  lower mass of  ozone, especially  at the  higher  power
settings.  The ozone production levels for the  two  air  flow rates is shown in
Figure 25.   As  shown,  ozone  production  is nearly  the same  for  both air flow
rates at all generator power  settings, although  the higher flow rate generally
had a slightly higher ozone production level.  Apparently, the ozone air  temp-
erature change and hence ozone production was not significantly affected  with-
in the range of  air flow rates  capable  for  the UTSD system.    The  fact that
little production difference was shown for the lower air flow rate is signifi-
cant, because a  smaller and/or  slower  speed air  compressor could  have been
used which would have resulted in an electrical  power savings.
                                       SCFM  AIR  FLOW
                                  o=47 SCFM  AIR  FLOW
           40    50   60   7O    80    90   100   110   120  130  140   15O
                        GENERATOR  SETTING - AMPS

   Figure 25.  Ozone generator production at various generator power settings
               (Ib/day x 0.0189  = kg/hr); (scfm x 1.70  -  cu m/hr).
                                     121

-------
     The ozone production levels shown in Figure 25 ranged from 7.7 kg/day (17
Ib/day) to 26 kg/day (57 Ib/day),  and  a  fairly uniform increase in production
occurred for  each 10 amp  increase of the  power  setting.    The  maximum ozone
production level  was 26 kg/day  (57 Ib/day).   This  occurred at  the  air flow
rate of 79 cu m/hr  (47  scfm).   The maximum amp setting was  not  tested at the
design air  flow  rate  of 118  cu m/hr  (70 scfm),  because  the  ambient ozone
concentration within the building  became  too high on  that  test day  and the
ozone generator was  shut down.

     The maximum  ozone production  level of  26 kg/day (57 Ib/day) at 79 cu m/hr
(47scfm) air  flow was  25 percent less than the manufacturer's  rated value of
34 kg/day (76 Ib/day).   Based  on comparable results for other amp settings, it
is not expected that the ozone production  level at the design air flow of 118
cu ra/hr  (70  scfm) would be significantly  higher.   The reason  for  the lower
than design ozone production level was not known  and  is  still being  investi-
gated.   All  known influences  on  ozone  production were optimized  during the
ozone production  tests,  including  lowest achievable air dew point as  measured
by the Shaw meter and clean  (no  scaling) water  jacket.  Also, prior to produc-
tion  testing  the generator  was  thoroughly cleaned, all  electrode tubes were
removed and checked  for  damage,  and all tubes  were  replaced according to the
manufac turer's recommendat ions.

Ozone System  Power Requirements—
     One of the  advantages  considered in  the  selection  of ozone for  the UTSD
plant was on-site production.  On-site production  capabilities were felt  to be
desireable when  compared  to  chlorine and dechlorination chemical  costs and
chemical hauling  in  the  canyon roads which led to  the  plant. The initial cost
of  the ozone  generation equipment  and the anticipated power costs associated
with  the continuous  generation  of ozone  were considered  in this selection.
During  the  research, an evaluation of the ozone generation  power requirement
was made to determine  if the initial  cost  assumptions  were adequate.

     The UTSD ozone system  has  been  intermittently operated, and the typical
operating procedure  was  to  dose  at a rate  to insure disinfection.  No attempt
                                      122

-------
 was  made  to  optimize  ozone dosage.    As  such,  realistic  values  for  power
 required  to generate  adequate ozone to achieve disinfection were not obtained.
 However,  power consumption  over  the operating  range  of the  ozone  generating
 system were determined  (i.e.,. ozone generation "mapping").   Each major unit of
 the  ozone system were separately evaluated.   Presently, power  is consumed by
 the  air pretreatment  system,  by the cooling and seal water  system,  and by the
 ozone generation process.   In the future, an ozone destruct  unit  for  the con-
 tact basin off-gas will  add  to  the  power consumption.

     Power consumption  for the  air pretreatment system  included power for the
 air  compressor,  refrigerant  drier,  air drying tower heater,  pneumatic control
 system air compressor, and electrical  control  circuit.   The power requirements
 for  the  air compressor,  refrigerant drier and  air drying  tower heater  were
 most significant.  The  power requirement for the pneumatic  control  system air
 compressor and electrical  control circuit were  insignificant in terms  of total
 power usage, and were not  included  in  the power  consumption evaluation.

     The  air  compressor operated continuously and  used 8.35 kW of  electrical
 energy.   The air compressor  was designed to provide a nominal  118 cu  m/hr (70
 scfm) air  flow to the ozone  generator.   As  described, the unit  discharged 160
 cu m/hr (94 scfm) of air,  and the excess  air had to be  bled-off to avoid over-
 loading the air  drying  tower.  It  was  also determined that  generator produc-
 tion did  not  significantly  change  from an air  flow  rate of  118 cu  m/hr  (70
 scfm) to  a lower rate of 79  cu  m/hr (47  scfm).
     The instantaneous  power  consumption of the refrigerant drier was 2.0 kW.
However, a  lower average  daily  power consumption was  determined because the
drier operating  time varied with the inlet air  temperature and air flow rate
to the drier.   As  described,  inlet air  temperature  increased  as the air com-
pressor seal water pressure decreased.   Generally, the average  inlet air temp-
erature was about 33°C.   The  relationship between the refrigerant drier oper-
ating time  and  inlet  air  temperature for  an  air flow rate  of  79 cu m/hr (47
scfm) is  shown  in  Figure  26.    At an  inlet air  temperature  of  33°C.,  the
average  refrigerant  drier  operating  time  was  11.1   hrs/day.   A  similar

                                      123

-------
DRYER OPERATING TIME - HRS /DAY
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            26   28   30   32   34   36
              INLET AIR TEMPERATURE -t
        Figure 26.   Refrigerant drier
        operating time at various in-
        let air temperatures and an air
        flow rate of 79 cu m/hr (47
        scfm).
evaluation  for the  higher flow  rate of
118 cu m/hr  (70  scfm)  indicated an aver-
age operating  time of 14.4 hr/day.  These
operating times were coupled with the 2.0
kW  instantaneous  power  consumption  to
determine  the  average  daily  power  re-
quirements of  the refrigerant drier.

     The air drying  tower used  electrical
energy  in  the tower regeneration cycle.
During  regeneration  the tower was heated
by an  electrical heater that  had an in-
stantaneous  power requirement of  3.65 kW.
The  8-hour  regeneration cycle consisted
of   tower   "heating"  for   4  hours  and
"cooling" for  4 hours.   During  the 4-hour
heating   cycle,   heater  operation  was
controlled  by a  high  temperature  cut-off  and  a  lower  temperature  start-up
system.   Therefore,  actual  heater  operating time  was less  than  the total  4
hours.  The  average  heater operating time per heating cycle  was determined to
be 3.25 hours, resulting in  a daily average  electrical usage  of 1.48 kW.

     One other use of  power  for  the ozone  system  was  supply water  for  ozone
generator  cooling  and for  air  compressor  operation.   This water  was provided
by  the plant potable  water pumping system.    A special  power  consumption
measurement  taken to determine the  power usage of  the  potable  water  system
indicated  that the average  daily power  consumption was  2.2  kW.    The potable
water  demand for the ozone  generation  operation was  about  95 percent of  the
total  plant potable water usage.   Therefore,  the power  required  to  supply
water  to the ozone generation system was 2.10 kW.

     Air pretreatment power  consumption data is  shown in Table 31.  The  daily
average power consumption for  the air  compressor and air drying  tower  heater
was  not affected by  air flow rate.   Power consumption of the refrigerant  drier
124

-------
was  affected by air  flow  rate.   However,  the net  effect  was that  the  daily
average power consumption  was  not significantly different  for the two air flow
rates.
      TABLE 31.   SUMMARY  OF  POWER CONSUMPTION FOR THE AIR PRETREATMENT
                  AND COOLING WATER UNITS
    Unit
  Ins tantaneous
Power Consumption
  Daily Average
Power Consumption

Air Compressor
Refrigerant Drier
Air Drying Tower
Cooling and Seal Water
TOTAL

(kW)
8.35
2.00
3.65
5.00
	

@47 scfm
(kW)
8.35
0.93*
1.48**
2.10***
12.86
USE 12.9
@ 70 scfm
(kW)
8.35
1.20*
1.48**
2.10***
13.13
USE 13.1
   scfm x 1.70 = cu m/hr.
  *Refrigerant Drier on-time at an average  inlet  air  temperature  of  33°C.
 **Average drying tower heater on-time of 3.25 hours  per  8-hours  cycle.
***Average potable water pump on-time of 10.5 hours.   (95% of  potable  water
   used for cooling and seal water).
     The power  requirement of the  ozone  generator increased  as  the level  of
ozone  production  increased.   The  most important  consideration  was the  power
required to produce a given mass of ozone (i.e., power utilization  in terms  of
kWh/lb).   Two  different  air  flow  rates  were  used in  determining generator
power  utilization,  and power  consumption measurements  were  taken  at  10 amp
intervals starting where  reliable  and reproducible ozone production began (40
amps) and were continued  to the generator's maximum setting  (150 amps).
     Power consumption for  the  ozone generator had to be carefully determined
because power consumption measurements for the air pretreatment and the gener-
ator were combined in the readings obtained from the single ozone system watt-
hour meter.  In order to attain the  power consumption for the ozone generator
the power consumed by the  air pretreatment units  that  were  operating at that
time was subtracted from the  total measured  ozone  system power that was indi-
cated by the watt-hour meter.  Using this procedure, reproducible ozone gener-
ator power consumption values were obtained.
                                      125

-------
     The   ozone  generator   production,
power consumption and power  utilization
values  for the  two  evaluated  air  flow
rates are  shown in Table 32.   Generator
power consumption varied from  a low  of
4.4 kW  to  a high of 25.1 kW  as  the  gen-
erator   amperage   setting   increased.
Ozone production also  increased as  the
amperage increased,  but  at a  lesser  rate
than  power consumption  as  evidenced  by
the   increase   in   power  utilization.
Power utilization increased  from a  low
of 13.7 kWh/kg  (6.2  kWh/lb) to  a high of
23.6  kWh/kg  (10.7   kWh/lb),  which  is
graphically illustrated  in Figure 27.

     The power  utilization values shown
in Table  32  for Ozone  Generator No.  2
were  obtained   under   conditions   that
would  yield  maximum  ozone   production.
These conditions  include:  air  dew point
equal to or less than -70°C  as  measured
by the  Shaw meter,  all  electrode tubes
                                              24
                                              22
                                            CD 20
                                               '8
                                             i  16
                                            Z
                                            o
                                            -  14
                                               io
                                            DC
                                            111
                                            5
                                            o
 GENERATOR  PLUS
|AIR PRETREATMENT
 AND COOLING
                                                   GENERATOR ONLY
                                                       0 = 47 SCFM AIR FLOW
                                                       A=70 SCFM AIR FLOW
                                                0    10  20   30   40   50   60
                                                 OZONE PRODUCTION - LB/DAY
                                            Figure 27.  Measured power utili-
                                            zation for the existing UTSD ozone
                                            generation system (scfm x 1.70 =
                                            cu m/hr; Ib/day x 0.454 = kg/day,
                                            kWh/lb x 2.21 = kWh/kg).
operational, negligible  scaling of  the cooling  water  jacket  and  a recently
cleaned ozone generator.   It should be noted  that  a series of power  utiliza-
tion measurements were  taken before Generator  No. 2  was  cleaned.   The un-
cleaned generator power  utilization was an  average 15  percent  greater  than
values that are presented for  the cleaned generator.

     A summary of  the  total  ozone  system power requirements for each  air  flow
rate evaluated is  shown  in Table 33 and 34.  The power utilization values for
the  two air flow  rates  were  compared  graphically  in  Figure 27.   As  shown,
power utilization  for  the two air  flow rates was not significantly different.
Apparently, the difference in air  flow rates which represented a fairly broad
                                      126

-------
                 TABLE 32.  OZONE GENERATOR POWER REQUIREMENTS
Ozone Generator
Ozone Production

Amperage
(ampere)
40
50
60
70
80
90
100
110
120
130
140
150
@
47 scfm
(Ib/day)
16.8
22.8
27.4
31.5
35.1
	
43.1
45.9
50.0
51.8
55.4
56.3

-------
r
                  TABLE 33.  TOTAL OZONE SYSTEM POWER REQUIREMENT AT AN AIR FLOW OF
                             79 CU M/HR (47 SCFM)
Generator
Power
Setting
(ampere)
40
50
60
70
80
90
100
110
120
130
140
150
Ozone
Production
(Ib/day)
16.8
22.8
27.4
31.5
35.1
	
43.1
45.9
50.0
51.8
55.4
56.3
Power Consumption
Generator Support Systems Total
(kW)
4.4
6.2
7.8
9.7
11.4
	
15.1
17.0
19.7
21.4
23.5
25.9
(kW)
12.9
12.9
12.9
12.9
12.9
	
12.9
12.9
12.9
12.9
12.9
S2.9
(kW)
17.3
19.1
20.7
22.6
24.3
	
28.0
29.9
32.6
34.3
36.4
38.8
Power
Utilization
(kWh/lb)
24.7
20.1
18.1
17.2
16.6
	
15.6
15.6
15.6
15.9
15.8
16.5
            *Air Compressor - 8.35 kW, Refrigerant Drier
             Heater - 1.48 kW and Cooling Water Pumping =
=  0.93 kW, Air Drying Tower
2.10 kW.
                  TABLE 34.  TOTAL OZONE  SYSTEM POWER  REQUIREMENT AT AN AIR FLOW OF
                             118 CU M/HR  (70  SCFM)
Generator
Power
Setting
(ampere)
40
50
60
70
80
90
100
110
120
130
140
150
Ozone
Production
(Ib/day)
17.1
22.9
	
32.5
36.2
40.0
43.9
47.2
50.3
53.9
56.8
____
Generator
(kW)
4.6
6.4
	
9.9
11.4
13.1
15.1
17.2
18.8
20.8
22.6

Power Consumption
Support Systems
(kW)
13.1
13.1
	
13.1
13.1
13.1
13.1
13.1
13.1
13.1
13.1

Total
(kW)
17.7
19.5
i 	
23.0
24.5
26.2
28.2
30.3
31.9
33.9
35.7

Power
Utilization
(kWh/lb)
24.8
20.4
	
17.0
16.2
15.7
15.4
15.4
15.2
15.1
15.1

              Ib day x 0.454  - kg/day;  kWh/lb  x 2.21  =  kWh/kg
            *Air  Compressor  =8.35 kW, Refrigerant Drier  =  1.20  kW,  Air  Drying  Tower
              Heater = 1.48 kW and Generator Cooling  Water = 2.10 kW.
                                                   128

-------
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 less  efficient electrical  energy  usage
 occurs at lower ozone production require-
 ments.  The fact that  the  power utiliza-
 tion   increases   dramatically   at   low
 production requirements  has  significant
 impact when applied  to wastewater  treat-
 ment plant operation.

      At  the  UTSD  plant,  variations  in
 wastewater volume  and  effluent  quality
 occur.    Although  flow  equalization  is
 available, plant flows have ranged  from
 1140 cu m day  (0.3 mgd) to  3,780 cu m/day
 (1.0 mgd).  To optimize ozone dosages  in
 line  with  these  flow  variations,   an
 adjustable ozone  generation system  is
 required.   The  present  system at the  UTSD
 facility  is  adjustable  by  varying  the
 amperage setting but  at low ozone produc-
 tion operating requirements,  the  system
 operates in the least  efficient  electri-
 cal  energy usage range.
     Similarly, municipal  wastewater treatment  plants  are typically designed
for future and larger flow rates.  Also, most of these  facilities are designed
without  flow  equalization  capabilities.    As  such, lower  ozone  production
requirements will  most likely occur  during the  design life  and  even during
diurnal periods.   At a lower ozone production requirement, the power utiliza-
tion value could be much greater  than at design production levels which would
result in  operation of a  proportionately less  economical  ozone disinfection
system than would  occur at  design flows.  The need  for economical  ozone pro-
duction over an adjustable range  exists.   In order  to  have this flexibility a
more uniform power usage efficiency must be developed.  Multiple ozone genera-
tion and/or multiple air pretreatment units should be  considered in  order to
    O   10  20  30  4O  SO  60  70  SO
       OZONE PRODUCTION - LB /DAY
Figure 28.  Comparison of equip-
ment specifications and actual
UTSD ozone generation system power
utilization (scfm x 1»70 = cu m/hr) ;
Ib/day x 0.0189 = cu m/hr; kWh/lb
x 2.21 = kWh/kg.
                                      129

-------
achieve more uniform power utilization values  for  a broad range of ozone pro-
duction requirements that  can be expected to  occur with municipal wastewater
treatment facilities.

     The UTSD  ozone system  was intermittently  operated because  of periodic
high ambient ozone  concentrations in the plant  working environment.  Several
modifications  to  the ozone piping and contact basin were made  to reduce the
ambient ozone  concentration  when the generators were operated.  One remaining
modification is an  ozone destruct unit for the  off-gases from the ozone con-
tact basin.  This unit  has been designed and is being constructed, and  repre-
sents  another  source of  power  consumption associated  with  the ozone system.
The expected power  consumption  is between 8 and  17  kW.

March  1979 Update—

     During the data collection phase of  the  research project  the  dew  point  of
the air from  the USTD  ozone generator  air pretreatment  system was  measured
with a Shaw Model "S"  Mini Hygrometer which had a  red spot  probe.  This data
indicated  that the  air  pretreatment system worked  well in that the dew point
of  the air varied  from -74°C to -54°C,  where -51°C  was the dew  point  recom-
mended by  the  manufacturer.   However, subsequent to  the data  collection phase
of  the research effort, new  information  was  recieved that indicated  that  the
Shaw dew  point meter may be giving  inaccurate readings(6).  Subsequently,  the
ozone  manufacturer  was  contacted regarding this item and consented  to sending
a dew  point cup measuring device to the  UTSD plant  for  purposes  of measuring
the dew point  of  the air from the air pretreatment system.    The dew point  cup
was received and  comparative dew point  readings were taken in  March, 1979.

     A diagram  of   the  dew  point  cup  measurement device  is illustrated  in
Figure 29.  As shown,  the air  stream is  directed  onto  the side of  a  polished
stainless steel cup that is  attached to  an outer container.   About 2.5 to 5 cm
(1  to  2 inches) of  acetone  is  placed  into  the cup and  ice is  slowly  added to
the acetone until  water in the "dry air"  stream  condences  on  the  polished
stainless steel.  A thermometer that had been placed into the acetone/dry icer

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mixture is then read, and the  tempera-
ture  reading  at that instance is the
dew point  reading of the  air stream.
Using   this    procedure   reproducible
results were obtained and were consid-
ered to be quite accurate measurements
of the air dew point.  (Note:  A mini-
mum amount of  tygon  tubing  is used to
pipe the air flow to the dew point cup
to avoid  possible moisture  uptake in
the tygon tubing.)
                                                    THERMOMETER
                                               OUTLET
                                               POLISHED
                                              STAINLESS
                                             STEEL CUP
                                             OBSERVATION
                                                 WINDOW
                                                                     INLET
                                                                 OUTER
                                                                 'CONTAINER
                                             Figure  29.   Schematic Diagram
                                             of  dew  point cup  air dew point
                                             measuring device.
     The  dew point results  using the
dew point cup were  found to be signi-
ficantly higher than the results using
the Shaw Mini Hygrometer,  as shown in
Table 35.   The dew point  cup results
ranged 42°C,  from -53°C to -11°C, while  the Shaw meter  readings ranged  only
-6°C, from -74°C to -68°C.   The Shaw  meter-definitely was not as  sensitive  as
the dew point cup.  More importantly  however, the Shaw meter  results  indicated
that dew point levels for the air pretreatment system were better  than minimum
acceptable levels  of  —51°C specified by  the ozone  manufacturer.  Conversely,
the dew point cup results indicated that  the dew point was usually higher  than
the desired minimum value of -51°C.

     Based on this  new information of  the  actual  dew point  of  the  air being
greater than specified  by the  ozone  manufacturer,   different conclusions are
indicated for some  of the information  presented  in the  text of  this report.
Some conclusions  remain  essentially unchanged  and  still other new conclusions
are dictated.  The  remaining discussion is  presented with  respect to the new
and more accurate dew point information.

Generator Flooding—  As  discussed,   several  occasions  of  generator flooding
occurred.  In order for this condition  to occur, the air  drying  towers must  be
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saturated  condition,  the  desiccant material in the towers loses  effectiveness
as  a drying agent.   It is  suspected that  the  desiccant in  the UTSD drying
tower is ineffective.  New desiccant  material  has  been  ordered.

           TABLE 35.   COMPARATIVE DEW  POINT  READINGS OF  DEW POINT  CUP
	VERSUS SHAW MINI  HYGROMETER,  MARCH 15.  1979
   Drying Tower
  Operating Time
      (hr)
           Air Dew Point
Dew Point Cup   Shaw Mini Hygrometer
    Ozone*
Concentration
  (ppm/vol)
0
1
2
3
4
5
6
7
8
-42
-53
-41
-34
-26
-19
-15
-12
-11
-72
-74
-74
-72
-72
-70
-69
-68
-68
«
2683
2756
2648
2621
2502
2368
2314
2195
2170
    *0zone  concentration using Dasihi  Meter.   Generator  air flow was  118  cu ml
     hr  (70 scfm).

     The generator flooding problem was  associated with four major  items;  1)
continuous  overloading of the  air drying  towers,  2) sticking of  the linkage in
the tower switching mechanism, 3) refrigerant drier failure  and, 4)  low  water
flow  to  the water  ring  compressor due to plugging of  an in-line  filter  that
could not be detected due to improper placement  of an in-line pressure gauge.
The cause of the refrigerant drier failure was  unknown.   It is  now  suspected
that  the failure was due to  an extreme  high temperature  oveloading problem
caused by item number 4  above.  Of all the above mentioned  items,  item number
2  was  most   directly  related to operational  considerations.   The  other  items
were  related  to  the design arrangement  of  the  ozone system purchased  as  a
                             &
package  unit from  the manufacturer.   These  items  have  now been corrected  by
installing  an air flow valve after the air compressor  and before the  refriger-
ant  drier  and  air  drying towers,  and by placing  the  pressure  gauge used  to
indicate the pressure  of the  water to  the water  ring  compressor  at a  point
after the inline  filter screen.
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Dew  Point  Monitoring— A conclusion  was reached that  a method of  monitoring
the  dew point and sounding  an alarm for a high dew point level was  necessary.
This  conclusion is  now more valid  than  ever.    In addition  to  preventing
generator  flooding,  it would also have  reduced  the rate of desiccant  failure
that apparently has  occurred  at  the UTSD plant.   However, in view of the  poor
accuracy of  the Shaw  dew  point meter,  an  expanded aspect  of  the  conclusion
that a dew point meter and alarm should be provided, is  that  a dew point  cup
measuring  device should also be  provided in -order  to  properly calibrate  the
dew  point meter and/or  properly  set the  dew point high level alarm.

Generator Production Verses Dew Point—'The  Shaw dew point meter indicated  that
the air dew point was  always  better than the manufacturer's minimum  acceptable
level of -51°C.  The later obtained dew  point cup  results  indicated that  the
opposite was  true,  and thus  the air pretreatment  system was  not functioning
satisfactorily.  The ozone production results did  change when the Shaw meter
indicated a change in  dew point, but the  actual dew point values were probably
higher  than  the minimum acceptable  levels.    A quantitative  figure  of  the
actual dew point values was not obtained, but values of 30 to 40°C higher  than
minimum acceptable levels  may have occurred.  The  conclusion  that ozone  pro-
duction changes as dew  point  chnages is  still valid, but for a different range
of dew  point values than  indicated previously.    It  should  be  noted that,
according  to  the  ozone equipment manufacturer,  ozone  production does   not
change appreciably when the actual dew  point  is  lower that  -51°C.   This could
not be verified at the UTSD plant, but hopefully will be when  the new desic-
cant material is installed.

     The conclusion  that ozone dosage will  vary during a  drying  tower cycle
along with the recommendation that accompanied  it,  was  extremely critical  for
the actual air dew point levels experienced.  They are less critical if gener-
ator production does indeed change only slightly during a typical drying tower
cycle, when the actual  dew  point level  is always lower  than 051°C.   However,
the  concept of  the  conclusion  and associated recommendation still  is  valid,
and  it  is  still felt  tha  much  benefit would be  derived if  ozone  generator
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manufacturers would provide specific, or at least a range of generator produc-
tion values for various power settings and dew point levels for their particu-
lar systems.   This information would  greatly aid design  engineers in system
design, and also  would be extremely beneficial  to  plant operators since they
would be  able to periodically check their  system's  performance with expected
values.   In so doing,  minor problems may be  corrected  if  the system perform-
ance was  noted to be  poorer than  expected,  and  corrective  action initiated
which may prevent major and more costly problems from occurring.

The maximum ozone production level of the UTSD  generator  was 1.26 kg/day  (57
Ib/day); which was 25% less  than  rated by the manufacturer.  The major reason
for the lower ozone production  level is now attributed to  a  low actual  dew
point of  the  air  fed to the  generator.   It  is not known if the generator will
meet  or exceed production  specifications when  the drying  tower desiccant  is
replaced  and  the dew point is lowered,  but certainly much better  performance
is expected.

Generator Power Requirements Verses  Dew Point—The  actual power  utilization
values  obtained during the research project were greater than  expected design
values, because the  ozone production rate was lower than expected.  It is  now
felt  that the major reason  for  the low producton levels was due to a higher
than minimum  acceptable dew point  of the air feed stream.  When  the dew  point
decreases,  the level of ozone production is expected  to increase  and  the  rela-
tive  power utilization values decrease.   However, this aspect was  considered
in  the discussion of  ozone  system power requirements.   Therefore, no  changes
in  the overall conclusion regarding ozone  power requirements  as  discussed  are
necessary.
 Ozone  Contacting  System—

      Ozone produced in the generators was directed to the ozone contact basin.
 Several design modifications were  made to  the  ozone contact  basin  and ozone
 piping arrangement.   Some of the modifications  represent "state  of  the art"
 design changes that evolved over the 2-year operation period of the UTSD ozone

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 system.   The modifications made  include:   contact  basin covering, basin  ex-
 haust changes, baffle  and  scum skimmer changes, and ozone piping and  diffuser
 replacement  and an ozone destruct  system.

     An  initial  obstacle in  operating the ozone  disinfection  system was  the
 presence of  high ambient ozone concentrations in the operator working  environ-
 ment.   Present minimum acceptable  standards  for human  exposure  to ozone  are
 0.1 ppm  by volume  for  a period not to exceed 8  hours.   During initial start-
 up, ambient  ozone concentrations of 3-5 ppm by volume for 2-hour periods, with
 peaks of 15-30 ppm by volume were  encountered.

     It was  determined that a portion of  these  high ambient ozone concentra-
 tions were the result  of a  partially covered contact basin.  Additionally,  the
 part of  the  tank which was covered was  not sealed.   The  contact basin  was
 modified by  covering the entire  basin with aluminum  plates and  sealing  the
 joints with  hypolon  gasket material.   It  was  anticipated that a  covered  and
 sealed basin would prevent  off-gas leaks.

     When the revisions were completed, ozonation was again attempted  but high
 ambient  ozone  concentrations still occurred.    This  problem was  isolated to
 ineffective  sealing  of the basin  cover.   A silicone  caulk was applied  in a
 continuous bead to obtain a positive  seal.   High ambient ozone concentrations
above the contact basin were reduced,  but were then detected in the main plant
 offices.   Off-gas  that  could no  longer  escape through  the basin  cover  was
being forced to  the  air space above  the  backwash  water  storage basin.   This
basin was  adjacent  to  the ozone  contact basin  and  below  the   main  plant
offices.  Additionally, contact basin off-gases were not being properly vented
 to the roof  discharge  because  foam produced  by the addition of air and ozone
 to the contact basin was blocking the exhaust air flow to the vent duct.
     To  correct the  problem of  off-gas  leakage from  the backwash  storage
basin, a duct connecting  the  existing ozone contact basin  with  the air space
above the backwash storage tank was installed.  The addition of the duct elim-
inated high  ambient  ozone concentrations  in  the plant offices,  because when
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foam blocked the movement of air  above  the  water surface of the ozone contact
basin the ozone  laden  off-gases would transfer  to  the  backwash water storage
basin where  they would  be  pulled back  into the main  exhaust duct  and dis-
charged.   This duct provided  an alternate  means for  ozone  laden air  to  be
removed when foaming occurred.   In addition to  the  duct modification, a water
spray nozzle was installed in the ozone contact  basin duct to depress the foam
as  it  developed.    It  should  be noted  that  the  excessive  foaming problem
occurred during ozone system start-up and typically lasted for only 2-3 hours.

     During  initial  operation of the  ozone contact system  it was determined
that short-circuiting of  flow was occurring across  the  top of the compartment
baffles.   This  short-circuiting  resulted when  air/ozone from  the   diffusers
"air-lifted" the water level in the  basin.   The baffles were raised  slightly,
but not to the extent that air movement to  the exhaust vent was blocked.

     The air-lift action  caused by the diffuser  system also caused flooding of
the scum skimmer mechanisms which were  initially set too low.  The adjustment
range of the  skimmer units was expanded  and adjustment handles were extended
through  the basin  cover.   To  facilitate  adjustment  of  the overflow weir
plates,  plexiglass  sight windows were installed into  the basin  cover above
each skimming unit.  To date, the continuous use of the  scum  skimmers has been
unnecessary  as  little foam or  the   predicted gelatinous type  froth  has been
produced.  The lack  of appreciable foam or  froth is believed to be due to the
high quality water entering the ozone contact basin.  This water has  very lit-
tle material (i.e.,  total  suspended solids) available  to  be coagulated into
froth.
     The  combination of modifications  allowed operation of  the  ozone system
whenever  the wind was blowing  sufficiently  to  remove  the ozone laden off-gases
from the  area surrounding  the  discharge stack.  The system bad to be shut down
when the  wind was not  blowing because high ambient ozone concentrations would
develop  in and  around the  plant area.    The  UTSD  was  instructed  by State
Department of Health officials to operate  the  ozone  system to achieve disin-
fection,  but the District  was allowed  to shut  down  the system when necessary

                                     136

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to prevent human exposure to high ambient concentrations of ozone.  Under  this.
arrangement, it  is  estimated that the  ozone  disinfection  system was operated
only about 50 percent of the time.

     The UTSD ozone  system  was operated under  these  conditions for about one
year when problems were encountered with the ozone diffusers and with leaks in
the ozone piping.   The  original ozone piping from the  generator  to the ozone
diffusers was Schedule  80,  U.P.V.C.  pipe with  both  solvent  weld and threaded
joints.   The  problems with leakage  occurred around  the  joints and along
straight pipe sections near  pipe hangers.   This leakage problem may have  been
caused by  inadequate care during  installation; however, good  plumbing prac-
tices by the contractor were felt  to  exist  because very few problems occurred
with other  plant piping systems.  Although no definite conclusions  could be
developed, the leakage  in the ozone  piping may have occurred  as  a result of
ozone exposure over a one-year time period and  not due to poor  workmanship.

     Because of  the  excessive  ozone  leakage of the D.P.V.C.  pipe, all piping
was replaced with Schedule 40,  Type  304 stainless steel.  Some of the stain-
less steel pipe  connections  were  threaded and some were welded.   Some of the
threaded stainless  steel  connections were  noted  to leak and  were tightened,
but some  could  not be  sealed  and were eventually  welded.   It was concluded
that welded connections provided the best assurance for sealing.

     When U.P.V.C.  piping  was replaced  new  ozone  diffusers  were also  in-
stalled.  The  diffusers were  connected to the stainless  steel  pipe  outside
the basin, and the pipe with diffusers was lowered into the basin aided by the
structural integrity of the  stainless steel pipe.   During  installation of the
diffusers an additional reason for replacing the U.P.V.C. piping with stain-
less steel pipe was noted.   Upon  removal  of the U.P.V.C.  pipe that  had been
submerged in the contact basin it was noted that  the  pipe  was  extremely brit-
tle and shattered easily when dropped.  The U.P.V.C.  pipe's  condition was not
felt to be acceptable for long-term  operation,  and replacement with stainless
steel pipe  was  considered appropriate.   These results indicate  that  strong
                                     137

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consideration should be given to using suitable grade stainless steel pipe and
welded connections for all ozone/air piping.

     The UTSD Ozone contact basin achieved ozone transfer efficiencies ranging
from 35 to 70 percent.   Transfer efficiency (TE) as used  in this context was
calculated   as    follows:
     TE
(Mass of Ozone Produced - Mass of Ozone in Off-Gas) (100)
                 Mass of Ozone Produced
     Typically,  the transfer  efficiencies were  between  50  and  60 percent,
which were considerably less than  the design TE of 90 percent.  One  reason for
the lower than expected TE was breakdown  of the ozone diffusers..  The original
ozone diffusers were tubuler in  shape and were attached  to a piping  connection
nipple with  a "2-part  epoxy bond".  The  epoxy served in a structural as well
as a  gas sealing capacity.   Because the  measured  transfer  efficiencies were
lower than expected,  the  contact basin was drawn down  and the diffusers were
inspected.   It was  noted that the epoxy  had become  extremely  soft.   The dif-
fuser  manufacturer claimed  that  the  epoxy would  probably become  "a  little
soft" when exposed  to  water.  A  new  diffuser was exposed to water  for 3  months
in the  laboratory.   No softening  effect was noted.  During  this  time  the  TE
had reduced  from  50 to 60 percent  to only about 35 percent.  The contact basin
was again drained and this time some diffusers were noted to have  completely
separated from the  connection  nipple and had fallen to  the bottom of the con-
tact  basin.

      The original ozone  diffusers  were  replaced.  The new ozone  diffusers were
porous  stone and  were  also  tubular in shape, but  a  bolted stainless  steel con-
nection and  hypolon  gasket material were incorporated  in  the diffuser con-
struction.   This  construction eliminates  the need for the two part  epoxy bond
which was not ozone  resistant.   Operation with  the new  diffusers has been
limited and  final conclusions concerning  the suitability of  the diffusers  has
not been reached.
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      After  installation of the. new ozone diffusers and stainless steel piping,
 TE tests  were conducted and were found to be similar  to efficiencies  that were
 attained  when the  ozone system was first started up, namely 50  to  60  percent.
 These values  were  better than the 35 percent efficiency attained when some  of
 the original  diffusers  were known to have failed,  but were still less  than the
 design efficiency  of 90 percent.   A re-evaluation of the ozone  contact  basin
 design was  made.

      The  UTSD ozone contact basin design was similar  to  a basin that was de-
 signed and tested  in 1971  at the Louisville,  Kentucky Wastewater Treatment
 Plant.    The  ozone  basin  at  Louisville  was reported  to  have consistantly
 achieved  90%  or greater  TE.  At  about that same  time at  the  University  of
 Louisville, research work was conducted to measure the  TE of a contact  basin
 similar to  the basin that  was  tested at the Louisville plant, and a paper was
 published concerning the  results.   The author reported that the 90% to 95%  TE
 that  was  achieved at the  Louisville plant could  not be duplicated at  the Uni-
 versity laboratory.   Laboratory  results  indicated a TE of  about  50%.   The dif-
 ference in  transfer  efficiency was  attributed to a "with reaction" consumptive
 use  of the  applied ozone at the Louisville  plant,  which was ozonating secon-
 dary  effluent.   The  phrase "with  reaction"  implies  that  the  effluent being
 treated had a high  ozone  demand  and that available ozone was consumed by this
 demand.   Thus TE appeared much higher because of this ozone demand.  The tests
 completed at the University of Louisville, which did not correlate with Louis-
 ville plant results, were  labeled  "without reaction"  test results.   These
 "without  reaction"  tests  also correlated well with ozone/liquid gas   transfer
 theories.

      Transfer efficiencies  achieved at  the  UTSD  facility have also correlated
 well  with ozone/liquid  gas  transfer theories, and are believed  to  be  more in
 line  with the  "without  reaction" tests conducted at  the  University of Louis-
ville.  The wastewater ozonated  at  the  UTSD  plant  is  tertiary effluent and of
 considerably better  quality than  typically  associated with  secondary treat-
ment .
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     The belief that the DTSD ozone  contact basin was performing similarly to
the "without  reaction"  tests as  established at the  University  of Louisville
was  further  supported.    Periodically,  the  ozone  transfer  efficiency  has
reached a  level  of about 70 percent.   When this  occurred,  poor disinfection
results  were  often achieved  even  if  disinfection  previously occurred  at
similar ozone  dosages.   At the same  time,  the TSS  concentration through the
basin increased.   This condition  existed when the ozone generator was started
after being shut  down  for a day or  two.   The  air pretreatment  system was
always operated, thus air was continuously  diffused  into the wastewater.  When
the ozone  generator was shut off  or  was operated at a very  low ozone dosage
level, biological  growth developed in  the basin in the form of a slime on the
basin walls, the U.P.V.C. baffles, and other surface  media in  the basin.  When
the ozone  generator was started and operated at a  higher ozone dosage, a  "with
reaction"  ozone consumption probably occurred  and  increased the  ozone  transfer
efficiency to  near 70%.  At  the  same time,  the biological slime would slough-
off and increase the contact basin effluent TSS concentration  which  interfered
with the disinfection capability  of  the system.  However,  when  the UTSD  ozone
contact  basin is operated on a continuous  basis it  is expected that it will
operate according  to gas/liquid  transfer theories.   It was concluded  that the
basin  is  achieving expected  ozone  transfer  efficiency  for  the  quality of
effluent  treated.    Based on  these  developments,  design  considerations for
desired  ozone  contact basin  transfer  efficiencies  should  be  based  on
ozone/liquid  gas transfer  theories.

     Biological  slime build-up occurs  in the' UTSD ozone contact  basin when the
ozone generator  is shut  down and/or  operated at a very low ozone dosage  level.
Because  of this  problem  with intermittent ozone operation,  a  good disinfection
versus  ozone dosage relationship was not obtained.   When  continuous  ozonation
and continuous good disinfection  is  achieved,  the ozone dosage will  be adjust-
ed to determine  the minimum  level necessary to achieve disinfection.   Transfer
efficiency tests  will  be made  to  determine  the  effective  ozone  dosage as
opposed  to applied ozone dosages  (i.e.,  dosage excluding  the  ozone lost  in the
off-gas)  so  that  a common basis  of  comparison can  be made  with other  ozone
disinfection systems.

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     To  achieve  continuous  ozonation,  several  options  were  considered  to
control the off-gas  ozone  discharge.   Among these were:  heat destruct, heat/
catalyst destruct, activated carbon,  recycle to sludge, and discharge  through
a tall stack.   The option  selected was heat/catalyst destruct.  Heat destruct
was  rejected because  of  an excessively high  power consumption.   Activated
carbon  was rejected because of  its  explosive  potential when  combined  with
ozone.   Recycle to  sludge and discharge through  a tall  stack  were rejected
because they were felt to  likely result  in  transferring  the problem  to  another
area  within the  plant.    The  heat/catalyst ozone destruct  system for  the,
contact  basin   off-gases has been  designed and  is being  constructed.   The
system is  manufactured by  Emery Industries.   An  off-gas  ozone  destruct  unit
should be  strongly considered for all  newly designed ozone systems.

     In March,  1979, the off-gas destruct  unit  was installed and operated for
only a short period  of time, because a 0.39 kW (1/2 hp)  fan motor.used  to  draw
the off-gas through  the destruct unit  burned  out.   The smaller motor is being
replaced with a 0.75 kW (1  hp) motor.  Preliminary indications are that  the
off-gas ozone destruct unit satisfactorily  reduced the ozone concentration  in
the off-gas to  satisfactoy levels  to  allow continuous  operation of  the ozone
system.   Quantitative information  was not obtained,  but from  a  qualitative
stand-point the system was acceptable.

Disinfection  Performance—
     Operation of the ozone disinfection system at the UTSD plant was sporatic
due to a variety of  problems that  resulted in  high ambient  ozone concentra-
tions representing a hazard to operating personnel.  Shown below is a synopsis
of the problems encountered.
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   Time Period
June - December, 1976
                       Comment

High ambient ozone concentrations due to
partial cover over contact basin.
December, 1976 - February, 1977    Good disinfection achieved, but equipment
                                   to measure ozone dosages and transfer ef-
                                   ficiencies not available.
March - April, 1977
May - June, 1977
Good disinfection achieved.

Poor disinfection achieved because of ozone
diffuser problem.
July - October,  1977
System shut down for inspection and repair
of original ozone diffusers.
October - December,  1977
Relatively good disinfection, but only with
extremely high ozone dosages because of
further  problems with ozone diffusers.
January  - April,  1978
Design, construction and  installation of
new  ozone  diffusers completed.
May  -  September,  1978
 Sporatic  operation  due  to  excessively  high
 ambient ozone  levels  in and  around  the
 plant  area  due to high  ozone concentrations
 in contact  basin exhaust.  Plans  and speci-
 fications for  off-gas ozone  destruct system
 developed.
      Routine collection of analytical data for  the  ozone  system was initiated
 during the week of December 12, 1976.  Results from these analyses for the en-
 tire research  period  are shown in  Appendix  F.   The  majority of  the  results
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 shown are weekly arithmetic  averages  of  data  collected  based  on  the  analytical
 schedule that was  presented  in Table  13.   Coliform results  shown in  Appendix  F
 are  weekly  geometric  means  of  the  individual  coliform  determinations.
 Coliform  data  was  developed   using the membrane  filter   (Gelman   Filter)
 technique through  the  week of April  10,  1977.  Results  after April 10,  1977
 were developed using the Most Probable Number (MPN) technique.

     In  general,   good disinfection  performance  could  be  achieved  when  the
 ozone diffusers were in  good condition and the system was operated  for an  ex-
 tended period of time  (several  days).  Disinfection performance was poor when
 problems were occurring  with diffusers and when the ozone system was operated
 on an  intermittent basis.   A summary of  performance data for  selected  time
 periods is  shown  in Table 36.   Periods  1,  2 and  3  represent data collected
 when the original  ozone  diffuses were in operation.  Period 4 represents data
 collected after the new diffusers were installed.

     During the 8-week time  period  for Period 1,  the original ozone diffusers
 were new and were  operating satisfactorily.   Very good disinfection occurred
 at an average applied  ozone dosage of about 11 mg/1.  The effluent- fecal coli-
 form concentration was reduced  to 30  per 100 ml, much  better than the design
 standard of 200 per 100 ml.  The COD  reduction during Period  1 was  12 percent
 and the TSS reduction  was  36 percent.  Both  the influent COD and TSS concen-
 trations were relatively low at  30 mg/1 and 5 mg/1, respectively.

     During Period 2 the average applied  ozone  dosage  was  about 9  mg/1,  but
 disinfection performance deteriorated significantly.  The effluent fecal coli-
 form concentration was 2,080 per  100  ml.   The reason for the  poor performance
was primarily attributed to  problems  with  the ozone diffusers.  During Period
 3  disinfection  improved,  but  only after  the  applied  dosage  was   more  than
doubled to about 1'9 mg/1.
     The performance data for Period  4  represents  information collected after
the new ozone diffusers were  installed.   The data was collected  for  two dif-
ferent time periods because of problems with intermittent ozone generation and
                                     143

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biological  slime  build-up.  Effluent disinfection  was achieved during Period
4.   The effluent  fecal  coliform concentration  was only  9  per 100  ml at  an
applied ozone dosage of about 7 mg/1.

     These  performance  data are limited, but  indicate that good  disinfection
can be achieved with  the  UTSD ozone system.   More  definitive conclusions are
expected when the  ozone destruct  unit  for the contact basin off-gas  is opera-
tional and  continuous ozonation can be  implemented.

SLUDGE DEWATERING  AND DISPOSAL

     Sludge dewatering facilities  are  provided at the Upper Thompson Plant  to
condition the  sludge  from the aerobic  digesters for  land disposal.    Process
operation  is  discussed  in  this  section.    Areas  investigated  included the
digested  sludge  characteristics,  design features,  and  initial  performance
data.   Results were  collected  during an  initial  start-up  period  and  then
through a 60-day testing period.

     Start  up of the Upper Thompson Plant began  in April,  1976; however, oper-
ation of the sludge concentrator did not  begin until nearly two years later  in
February, 1978.  This delayed operation was caused by  delays in finalizing the
design and  construction of portions of the sludge handling system.  Throughout
this two year period the waste sludge from the activated sludge system was ac-
cumulated in the two aerobic digesters.   This long  detention time resulted  in
a very well digested sludge, as indicated by  a specific oxygen uptake rate  of
less than 0.5  mg/hr/gm VSS and the volatile  solids to total  solids  ratio  of
less than 60 percent.  An  additional factor  that affected the digester sludge
occurred during the Big Thompson  flood  disaster (July 31,  1976).   A 76   cm
(30-inch) main  interceptor river crossing was washed  out and resulted  in  a
large amount of silt-laden water entering the activated sludge system.  Conse-
quently, the contents of the activated sludge process were wasted  to  the aero-
bic digesters.  The silt material  coupled with the  long sludge detention time
resulted in a large mass of inert material contained in the aerobic digesters.
                                     145

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     Because  of  the unusual  characteristics of  the sludge  to  be dewatered,
several tests were required to  select  the  most  suitable polymer.  A six place
paddle mixer  was  used to perform  standard jar  tests on  the digested sludge.
Several types  of  polymer were  investigated,  and once  a  specific polymer was
chosen   several   dosages   were   investigated    to   determine   the   optimum
concentration.  The polymer used through most of  the study was Nalco 627.

     During start-up  of  the sludge concentrator, a  major limitation with the
sludge feed system  to  the  concentrator was detected.   Because of head condi-
tions, the  sludge feed pump could  not maintain the flow rate. to the concen-
trator at a constant level.  With a varying sludge flow rate  the  desired poly-
mer dosage was difficult to maintain.   As  a result the characteristics of the
conditioned sludge  varied which  directly affected  concentrator  performance.
With  the  original arrangement, a  .diaphragm pump was  located in-line between
the aerobic digesters  and  the  sludge concentrator.   However, the  liquid level
in the digester was higher than the concentrator  which  created a positive head
on the sludge pump.   Sludge would  flow by gravity through the diaphragm pump,
limiting the pumps capability to control the  sludge  flow  rate.   As a result,  a
modification was  necessary.  As a  temporary solution,  a  1140 1  (300-gal) tank
was placed  inside the sludge handling  building  and  sludge from  the digesters
was allowed to flow by gravity to the tank where it  was then g.umped to the
concentrator.  This method  of  operation required the attention  of an  operator
to direct sludge  into  the 1,140 ml(300-gal) tank, but  it  did  insure a  constant
sludge flow to the  concentrator.   As a more permanent  solution,  a progressive
cavity pump was installed in place  of  the  diaphragm  pump  (March  1979).
     The  results  of initial  testing  on the sludge  concentrator are shown  in
Table 37.  The  testing  was  conducted in May, 1978, after the  sludge  feed  sys-
tem had been modified  to provide  a constant feed rate.   Although no  quality
tests on  the digested sludge were  performed for trial 2,  the  characteristics
should  have  been  similar  to those  shown in trial 1 since  the  digester contents
had  been maintained  for  such  a  long  time period.    During  the two  testing
periods the  solids  concentration of the sludge  cake  was 9.1 and 9.6  percent  by
weight.   Solids capture varied  from 78  to  82 percent,  whereas captures  greater
                                     146

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than 90 percent were expected..  The reason for the low solids capture was par-
tially  attributed to  the extremely  digested condition  of the  sludge being
dewatered.   It is noted  that the digester  contents had  a very  low  pH (4.2
units).   Sodium bicarbonate  was  added on several occasions to  attempt to in-
crease  the  pH but  bench scale  tests indicated  that much more  biocarbonate
would  be  required to  effect  the pH.    It was decided  to  dewater the sludge
already contained in  the  digester and to attempt  to control the  characteris-
tics of any future sludge through operational controls.

The average of the results for the two  trials shown  in Table 37 indicate that
approximately 110 Kg (245 Ib) of  sludge  (dry wt)  were fed  to the  concentrator
         TABLE 37.  SLUDGE CONCENTRATOR PERFORMANCE DURING START UP
                                                     Trial 1
                  Trial 2
Date
Duration — hours
Sludge Characteristics
  Total Solids - mg/1
  Total Voltile Solids - mg/1
  VS/TS Ratio - %
  Temperature - °C
  Specific Oxygen Uptake Rate mg 02/hr/gm VS
  pH - units
March 3, 1978  March 4, 1978
      4.9           3.8
     32,560
     17,760
      55
      29
      0.13          	
      4.2
Performance
Influent Flow Rate - gpm
Total Solids, Cake - %
Suspended Solids, Filtrate - mg/1
Sludge Feed Rate - Ib/hr (dry wt.)
Sludge Cake Produced - Ib/hr (dry wt.)
Sludge Lost in Filtrate - Ib/hr (dry wt.)
Solids Capture - %
Polyer Dosage - Ib/ton sludge (dry wt.)

15
9.1
4,480
245
190
55
78
39

15
9.6
2,770
245
200
45
82
41
  gpm x 0.0631 = I/sec; Ib/hr x 0.454 = kg/hr; Ib/ton x 0.50 = kg/metric ton
                                     147

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per hour, and with a solids capture of 80 percent, 90 Kg/hr (200 Ib) of sludge
cake (dry wt) was produced at a polymer dosage of 20 Kg/metric ton (40 Ib/ton)
of sludge.'  It is noted that  the  speed of the primary  and  secondary screens
had  to  be  carefully  controlled to avoid  solids loss  over  the  screen  edge
during these trials.

     Subsequent to these initial tests,  operation and performance data on the
sludge concentrator was  collected  over a 60-day  testing period  from August 1
to October  1,  1978.   A summary of this data  is  shown in Table  38.   Overall
performance during this  period was better than that  obtained during the ini-
tial testing period in May.  Additional operations experience was  felt to have
contributed  to the improved  performance.    During the  60-day  period, sludge
with an 11 percent solids content  was  produced which  yielded  18,900 kg (41,700
Ib) of dry  sludge solids.   To condition the sludge,  25  kg  (50  Ib) of polymer
per ton  of  dry solids was  required.   On the average  it  required 8.3 hours to
produce one metric ton of dry  sludge solids.

            TABLE 38.  SUMMARY OF  OPERATION AND PERFORMANCE DATA
Date
Duration - hr
Sludge Characteristics
  Total Solids - mg/1
  Total Volatile Soilds - mg/1
  VS/TS Ratio - %
  Temperature - °C
  Specific Oxygen Uptake Rate - mg  02/hr/gm VS
  pH - units
August 1, 1978 to October 1, 1978
                 192
              25,400
              14,660
                  58
               No Data
               No Data
                 5.5
Performance
Influent Flow Rate
Total Solids, Cake - %
Suspended Solids, Filtrate - mg/1
Sludge Feed Rate - Ib/hr (dry wt.)
Sludge Cake Produced - Ib/hr (dry wt.)
Sludge Lost in Filtrate - Ib/hr (dry wt.)
Solids Capture - %
Polymer Dosage - Ib/ton sludge (dry wt.)
20
11
2,070
254
217
37
85
50
    gpm x 0.0631  = I/sec;  Ib/hr x 0.454 = kg/hr;  Ib/ton x 0.50 = kg/metric/ton
                                     148

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     During  the  60-day testing  period,  an operation  problem was encountered
with  the  inlet  and  outlet flapper  valves on  the  sludge  feed  pump.    These
valves  collected pieces of  rags and  bits of plastic  from the  sludge.    The
valves  would  then not seat properly and the  flow would  slowly  decrease.   To
minimize this  problem,  the output of  the  pump  was checked  once  or  twice  per
hour, and  adjusted to maintain  a  75  1/min (20 gpm) flow.   During the 60-day
test period the  pump was taken apart  five  times  to remove the rag and plastic
build-up on  the  valve seats.  Approximately  30  min of  cleaning  time was "re-
quired  each time  the pump was taken apart.

     Additional  operational problems had to do  with maintaining a good sludge
floe.   It  was 'determined  that when  sodium  bicarbonate  was  added  and  the
digester sludge.  pH increased  to  greater  than  7,  the cationic polymer that  had
been used had little effect on flocculating the sludge.   Flocculation problems
also occurred when attempts  to  dewater sludge from  one  of the digesters  that
had not had any  waste  activated sludge added  to it  for 3 weeks  were made.
This sludge produced  such  a  poor floe that the primary  screen of the concen-
trator  could not  trap the floe particles.   When sludge was processed from  the
other digester that  had waste activated sludge  fed  to it  daily,  a  good  floe
was again achieved.

     The spray jets used to clean  the  primary and secondary screens also  pro-
vided some operational difficulties.   Plant effluent was used to supply water
to the  1.2-mm (3/64 inch)  jets, and  small particles  clogged the jets.    The
semi-plugged spray jets would not  adequately clean  the  screens.   To minimize
the plugging  problems,  the jets were  cleaned before each  6  hour filter run.
An inline strainer is being investigated to aid in trapping these small parti-
cles before  they entered  the spray jet.   The strainer should not have  to  be
cleaned as  often, and more  importantly the  effectiveness  of the  spray jets
would be maintained.
     During operation of  the  sludge concentrator,  water and solids (filtrate)
were returned  to the  plant headworks.   The  added water  is  from  the water
released from the sludge,  the water added by  the  inline  polymer diluter, and
                                     149

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water added  by  the jet cleaning sprays.   The water released  from the sludge
was about  57 1/min (15 gpm),  the water  added by the  inline  polymer diluter
about 30 1/min (8 gpm) and the water  required to operate the spray jets about
57 1/min (15 gpm)  for  a  total  volume of about 144 1/min (38 gpm).   Solids in
the filtrate result from  the  sludge  lost through  or over  the edge  of  the
travelling screens.  The filtrate  total suspended solids concentration during
the test  period averaged 2,070  mg/1.   The amount  of  solids  in the filtrate
varied directly  to  the dryness  of  the sludge.   The  highest  solids content of
the filtrate, 4,740 mg/1,  occurred with  a poorer sludge cake  of 9.4 percent
while  the  lowest  solids  of  344  mg/1  occurred  with a  good sludge  cake
of 12.1 percent.

     A cost  breakdown  for  the  60-day testing  period is shown  in Table 39.  A
total of 114 man hours was required  for operation of the sludge  concentrator.
This labor  included time  for start  up, operation,  maintenance  and clean up.
Electrical power to operate  the sludge dewatering  system was  estimated to be
176 kW/metric ton (88  kW/ton) of dry  sludge solids.   The cost was obtained by
multiplying  the  total  kilowatt consumption by the  UTSD power  cost factor of
$0.035/kW.   Sludge cake transportation included allowances for gasoline  and
the  drivers' time,  but insurance and  depreciation  on  the  truck  were  not
included.
            TABLE 39.  SUMMARY OF COST DATA FOR SLUDGE DEWATERING
Labor
114 man hrs.
x $5.00/hr -
$570
Polymer
1060 Ibs x
$1.221/lb =
$1,294
Power Costs
1830 kW x
$0.035/kW =
$64
Hauling
$60.00 labor (@ .58 hrs/ton)
15.92 gas (@ $0.65/gal)
$75.92 Total
                       Cost Per Ton Dry Sludge Removed
Labor:  $570 t 20.8 tons
Polymer:  $1,294 ^20.8 tons
Power - $64.06 - 20.8 tons
Hauling & Labor:  $60.00 t 20.8 tons
Hauling & Gasoline:  $15.92 •*• 20.8 tons
                                             TOTAL
                      $27.40
                       62.22
                        3.08
                        2.88
                         .76
                      $96.34/Ton Dry Sludge
Ib x 0.454 = kg; hr/ton x 0.907
  - metric ton
hr/metric ton; gal x 3.785 = 1; ton x 0.907
                                     150

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     The  total  cost  of sludge  dewatering  as  shown  in Table  39  was  about
$87/metric ton ($96/ton) dry sludge  solids.   The  labor and polymer costs com-
prised 93 percent of the total cost.

     The  sludge  concentrator was relatively  easy to  operate  once the proper
polymer  dosage  was determined.   The  full  attention  of  an operator  was  not
required and periodic checks were  all that was necessary.   Overall, the unit
performed well  despite  the quite  difficult-to-dewater  aerobically digested
sludge.   It  is  expected that even  better  performance in terms  of lower cost
and a thicker sludge cake can occur, when a less inert sludge is processed.

OVERALL TREATMENT PLANT PERFORMANCE

     The UTSD advanced  wastewater  treatment  facility functioned under a vari-
ety  of  operating  conditions  throughout  the data  collection  phase of  the
research project.   Plant flows ranged from.  30  percent to  134  percent of the
design flow (Note:  half plant design flow values were used because only half
of the  plants  major units  were  in  service).   The  BOD^  load  ranged  from 50
percent to 228 percent  of  design.   Despite  these  wide variations  'in loading,
overall plant performance  was  quite good.   A summary of  the  performance and
the effluent quality for each unit process for the period of the research pro-
ject is shown in Table 40.  It should be noted that  the effluent for each pro-
cess was  not sampled all  the time  during the data collection phase  of the
research  effort.   Initial  plant lab  start-up  problems  postponed individual
unit process analyses for  three  months until October  3,  1976.   Also, special
testing  for  the ozone  and denitrification  systems  was  completed during the
last two  months  of the data collection  effort  in place  of sampling and ana-
lyzing every unit process.  Thus, of 105 weeks of overall performance informa-
tion, 88 weeks of data  were  collected on all individual unit processes.   Data
presented in Table '40 is for this 88-week period.
                                     151

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                TABLE 40.  SUMMARY OF UTSD PLANT PERFORMANCE*
Parameter
Flow (mgd)
BOD5 (mg/1)
Removal (%)
TSS (mg/1)
Removal (%)
COD (mg/1)
Removal (%)
TKN (mg/1)
Removal
NH4-N (mg/1)
Removal
Alkalinity
as CaCOs (mg/1)
Removal
Influent
0.49
201
169
358
22.5
13.1
106
Activated
Sludge
Effluent
0.49
31
85
22
87
58
84
11.6
48
9.1
N/A
76
28
Nitrification
System
Effluent
0.49
34
83
21
88
55
85
8.6
62
5.5
N/A
49
54
Mixed Media
Filter
Effluent
0.49
11
95
6
96
35
90
6.8
70
4.9
N/A
45
58
Ozone
Contact
Effluent
0.49
11
95
6
96
35
90
6.4
72
4.8
N/A
45
58
   mgd x 3785 - cu m/day
  *Summary of data for 88 weeks from 10-3-76 to 6-10-78, excluding the 4-week
   period from 6-12-77 to 7-9-77 when modifications to the plant were
   completed.
     Although each parameter  could  be  discussed,  it is felt  that  BOD5 can be
used to indicate the variations in organic loading and performance that occur-
red throughout  the  project period.  The average influent  BOD5 concentrations
shown in Table 40 was 201 mg/1, indicating a typical domestic waste.  However,
further data evaluation  indicated  that an extreme  variation in waste strength
occurred.   The  winter  season  wastewater BOD^ concentration was  only about
100 to  150 mg/1, and  the summer  BOD5 concentration  ranged  from 250  to  400
mg/1.   The  BOD5 removal  efficiency  ranged  from  85  percent  to  98  percent
during  the course of  the study.   A  graphical  illustration  of  BOD5  removal
efficiency is shown in Figure 30.   The lower  removal efficiency of 85 percent
was attributed  to system start-up  conditions  after plant  modifications  were
made in June 1977.
                                     152

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     Also shown in  Figure 30 is the BODg  removal efficiency across  the  acti-
vated  sludge system.   As shown,  activated sludge  removal efficiencies  were
generally lower and  more  variable  during the beginning portion  of  the  project
and more consistent  and higher  toward  the  end.  More experienced process  oper-
ation by plant  personnel coupled  with changes in  system operation  that  were
earlier discussed were contributing factors to this occurrence.  It  should be
noted  that  lower overall plant 6005  removal occurred  near the very  end  of
the project  even  though  activated  sludge removal was  quite good.  The reason
for this  is due  to higher  BODg in the mixed media  filter  effluent  due  to
methanol addition during  the denitrification  special study.

     Many minor and  some  major  modifications  have been implemented  at the UTSD
facility.   These  modifications coupled  with  the  understanding  of  the  loading
conditions  that are associated with the UTSD facility should allow  continued
good and even improved process  performance.  As  such, the UTSD  should  be able
to maintain a high quality effluent.
                                           DENITRIFICATION SPECIAL STUDY
                                                        1-22
                                        1977
1978
    Figure 30.  Activated sludge and overall plant BODr removal  efficiency
                during the entire research project.
                                     153

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OPERATION AND CAPITAL COST

     The  plant was  constructed  in  1975  and  1976,  and  the  capital  costs
presented are  associated  with this period.   Total capital cost  for  the UTSD
treatment facility was approximately $3 million, or about $2 million per 3,785
cu m/day  (1 mgd)  of  treatment capacity.  This cost  includes  all subsequent
modifications made in the plant  design.   Data  on  the  operational cost of the
plant were  collected  during  the  research project.   The  average annual opera-
ting cost during  the  research project was $152,210.   Since the research pro-
ject required additional  manpower  effort,  this  cost is not reflective of nor-
mal  operation.   The  projected  annual  operating  cost,  excluding  research
project costs, was $123,000.   In the following  subsections  the overall capital
and operating  costs are broken down for each of  the specific unit processes.
A summary of individual process costs,  as well as total costs,  is  also pre-
sented.

Lift Stations

     Two  lift  stations,  Fish  Creek and Big Thompson, were used  to  pump the
collected wastewater to the treatment plant.  The  lift stations consisted of a
wetwell, dry-well, pumps  and  a comminutor  with  bar screen by-pass.  The  total
capital cost for  both lift stations was  $189,720.   The cost for  the pumps and
comminutors  comprised about $37,000 of this total.   Construction  materials and
labor  for the  lift stations  cost  an additional $80,000.  Piping, electrical
systems, equipment controls,  and site preparation  at $72,720 accounted for the
remainder of  the total  lift  station cost.    The capital  cost  of  the lift
stations was approximately 6.4 percent of  the total plant cost.

     Operational  cost for the various  treatment  processes  were  divided into
three  categories:  supplies,  labor and  power.   Supplies  for the  lift  stations
consisted mostly  of  lubricants for the  equipment.   Since this cost was  minor
compared  to  the total cost,  it has been included  in the  miscellaneous section
of this analysis.  Labor  used for  the inspection  and  maintenance of  the lift
                                      154

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stations was estimated  to  be  2.5  hours per day.  The annual  labor  requirement
was then computed as 912 man-hours, which  was  10.2% of  the  total  annual  staff-
ing cost and amounted  to  $5,016.   The power  requirement for the lift station
was based  on the  horsepower of the operating  pumps with respect to the  total
plant horsepower.   This percentage,  when used in conjunction with  the average
power cost for the  plant  of  $3,766  per  month,  provided an  estimate  of  the
monthly power cost.  The monthly  power cost for  the lift  stations was $107, or
$1,284 per year.   When the labor and power costs were  combined, the   annual
operation  cost of the lift station was $6,300.

Flow Equalization and Grit Chamber

     The capital  cost  of  the  flow  equalization basin and  grit removal  units
was $270,540, or  approximately 9.1  percent of the total  plant  cost.   Of  this
amount, $55,440 was the cost  of the  grit basin and related equipment, and  the
flow equalization basin and clarifier equipment.  Materials and labor utilized
in  the  construction  of  these facilities accounted  for  $116,730,  and  the
remainder  of  the capital  cost at  $98,370 was  the  result of  the associated
piping, electrical systems,  equipment  controls and  site  preparation.   It
should be  noted that site  preparation for the  UTSD  was a  significant   cost,
since much excavation work was done by blasting.

     The cost of  routine supplies for these units was  negligible and was  in-
cluded in the miscellaneous section of this analysis.   The labor cost associ-
ated with  these units  was  based  on  1.55  hours  per  day  for  inspection, grit
handling and scheduled  maintenance  for a  total  labor requirement of  565 man-
hours per  year.   The resulting labor  cost was $3,108 per year.   Based  on  the
horsepower requirements, the  preliminary treatment's share of  the  power cost
was $211 per month,  or $2,532 per year.   When  the power and labor costs are
combined,  the annual operation cost for preliminary treatment totaled $5,640.
                                     155

-------
Activated Sludge

     The activated sludge  system consisted of two aeration basins, two clari-
fiers, and  the associated mechanical  equipment.   The  estimated capital cost
for the activated  sludge system was $569,400, which accounted for about 19.2
percent of the total plant cost.  Equipment cost  including aerators, clarifier
mechanisms,  return and  waste  pumps and  blowers  was $119,680.    Construction
materials and labor accounted  for an additional $243,055.  Other  capital costs
at a total of $206,665 were  for  piping, electrical systems, equipment  controls
and site preparation.

     The cost  for  supplies was considered negligible for this process and was
included in  the  miscellaneous section.   During  the  research project  the man-
power requirement  for  process control and  sampling  of  this process was esti-
mated to be  3,107 man- hours per year.  The resulting cost  for  this effort was
$17,090.  A  series of control  tests were  performed by the plant  operators, and
the frequency  of this  testing varied from four to six  times  per day.  From  1
to 1-1/2 hours were  necessary to complete a set  of  control tests.  Additional
time was required to develop and analyze  the  data  and  to implement  the indi-
cated  process  adjustments.   Following the research project  the  frequency  of
performing   the  control  tests and collecting samples  for  this process was
reduced  to  twice per day,  thus decreasing the  manpower involvement  to 1,969
man-hours per  year and the  annual  labor  cost  to  $10,830.   The power  cost  for
the activated  sludge process system was based on  the horsepower  requirement  of
the blowers, turbines  and pumps.   The  percentage of the power  cost  attribut-
able  to  the  activated  sludge process was $1,126  per month.   Total operational
             •
cost  during  the  research project was $30,512  per year;  however,  following  the
project  the annual cost  decreased  to   $24,342  due to the  decreased labor
requirement.

Nitrification
      Components of the nitrification system  included  the  tower  with two types
 of media - redwood and plastic, the recirculation pumps, and a wet-well.
                                      156

-------
The  capital cost  associated  with the  nitrification system  was $366,760,  or
12.4  percent  of the  total  plant cost.   Of this  total,  the tower  structure,
media and pumps accounted  for $188,130.  Materials and labor for construction
of  the  system cost an  additional $17,200.   Other capital  costs  at  $161,430
were allocated  to  the piping, electrical systems, equipment controls  and  site
preparation.

     The major  operational costs  for  the nitrification  system  were based  on
labor  and  power .requirements.   An  average  of  0.34  man-hours per  day  were
necessary for  operation of  the tower  resulting in an annual  labor  cost  of
$682.  Most of  this time went to maintenance and inspection of  the  recircula-
tion pumps.  Only  limited  maintenance was required  on  the tower or distribu-
tion nozzles.   The power cost,  based  on the horsepower  of the recirculation
pumps with  respect to  total  plant horsepower,  was  estimated to be $552 per
month, or $6,624 annually.  The subtotal for operation cost of  the  nitrifica-
tion tower was an  estimated $7,306 per  year.

Filtration

     Major items within the filtration  system include the mixed-media  filters,
backwash storage basin, backwash wastewater storage basin, pumps and the chem-
ical feed system.

     Approximately 12.8  percent of the total capital  cost,  or  $378,510, was
allocated to the filtration system.   Cost of the filter units, backwash pumps
and  the  chemical  feed  system accounted  for $152,390.   Materials  and labor
included in the construction  of basins and the  filter  room were estimated  to
cost $74,200.   The remainder  of the  capital cost at $154,880 went  to the as-
sociated piping, electrical systems,  equipment  controls and site preparation.
     Although a chemical feed system was included in the filter design, chemi-
cal addition was not practiced  during  the  research project.   The major opera-
tional costs were  the  result of manpower  and  power needs.   The  manpower re-
quired was mainly for filter backwashing.  When the head loss through a filter

                                     157.

-------
reached a preselected level, an  alarm was sounded.   The  operator then trans-
ferred the nitrification  tower  effluent to a clean  filter,  and initiated the
approximately 15-minute backwash cycle  on the dirty  filter.   The frequency of
filter backwashing  varied considerably during  the research project,  but the
average backwash frequency  was  ten times per week.   Manpower  requirements of
1.25 man-hours per day were allocated for these activities.   This resulted in
an annual manpower  cost  of $2,508.   The  only power  cost  associated with the
filtration system was the demand by the backwash pumps.  This amounted to only
$108 per year.  Total operational  cost,  including  labor and power, was $2,616
annually.

Ozone Disinfection

     Components of  the  ozone system  include the  air pretreatment  equipment,
generators, contact basin and diffusers,  and the  off  gas  destruct unit.   The
capital cost  of this  system was $341,460, or 11.5 percent of  the total  plant
cost.  As discussed previously  in  the ozone evaluation section,  several  modi-
fications were necessary in the system design, the  most  important  being the
piping and diffusers changes ($14,380) and the  off gas  destruct  unit ($21,330)
addition.  The costs  associated with  these  changes  have been included within
the capital cost.   Approximately $160,300 of the  capital  cost  was  for equip-
ment including:   air  pretreatment equipment, ozone  generators, diffusers and
piping, ozone monitoring equipment,  and the off-gas destruct unit.  Materials
and labor utilized for construction amounted  to $48,740.   The cost for associ-
ated piping,  electrical  systems, equipment  controls and site  preparation was
$132,420.

     Operation of the ozone disinfection  system required about  $1,000  per year
for materials.  Most of  this  cost  went to the purchase of electrode tubes and
fuses.  Manpower was required for  daily inspection of the  air pretreatment and
ozone generation equipment.   An additional 180 man-hours  per year were neces-
sary for inspection and  cleaning the ozone generator units.  These  activities
required an average of 1.2 man-hours  per  day, which  resulted in an annual cost
                                      158

-------
 of  $2,354.   Determination of  the power cost  for  ozone generation was  diffi-
 cult,  since the unit  was  not continuously  operated.   Values  obtained  during
 intermittent operation were  used to extrapolate the power  costs  shown.   Costs
 shown  are based on continuous operation.  Since the off-gas  destruct  unit  has
 been recently  added to the system,  the plant power records  do not reflect this
 additional  cost.   Based on an 8  kW demand for the destruct unit,  a power cost
 was estimated  for off-gas destruction.   The power cost  for  the  entire  ozone
 system was  estimated to be $8,916 annually.   When the cost  of the materials,
 labor  and power were combined, the  annual  operational  cost  totaled $12,270.

 Sludge Handling

     Sludge digestion,  dewatering and disposal are included  in this category.
 The following  items make up the sludge handling process:   digester basins,
 aerators, blowers,  sludge pump, dewatering equipment and  the  sludge truck.
 The capital cost  for this  system  totaled $453,850,  or  15.3  percent  of  the
 total  cost.    Of  this amount, approximately  $120,970  went to the associated
 equipment,  and $169,350 was  directed  to materials and labor  for  construction
 of the structures.   Other capital costs of $163,530 were associated with pip-
 ing, electrical systems, equipment  controls and site preparation.

     Supplies  for  the  sludge handling system were, for the most  part, related
 to sludge dewatering and disposal.   The annual cost for  chemical polymer was
 $3,318, based  on dewatering 90 tons of  sludge (dry wt. basis) per  year.   Also,
 about  $184/year went to transportation of the sludge cake  to ultimate dis-
 posal.   Total  cost  for supplies were  then  $3,502 per  year.   The  manpower
 requirement for  sludge handling  was 2.8 man-hours/day or 1,018 man-hours per
 year,  for an annual  cost of  $5,599.   Most  of the  manpower requirement went to
drawing supernatant  from the aerobic  digesters  and to operation and mainte-
nance  of  the  sludge  dewatering  system.    The  power  demand  of the  sludge
handling system was  mostly  due  to  the operation  of the  aerators   and the
blowers.   An annual cost of $8,616 was allocated for the power requirements of
sludge handling.    The total  operation cost, including  supplies, labor and
power,  was $17,717 per year.

                                     159

-------
Miscellaneous

     The remainder of  the  total  capital cost of the  plant,  $391,470,  was in-
cluded  in a  miscellaneous  category.    The plant  laboratory  and  associated
equipment accounted for $59,630, and $331,840 went to material and labor costs
for the  plant administration and control building.   Major equipment included
in the main  plant building included the  standby  generator,  non-potable water
supply system, and the heating and ventilation systems.

     The majority of the plant expenditures for supplies could not be specifi-
cally  divided among  the previously discussed processes;  consequently,  they
were presented in  this subsection.   Items  included within this category were
the following:  operation supplies, repairs and maintenance, insurance, natur-
al gas,  lab  chemicals,  telephone,  transportation,  equipment rental and office
supplies.    The   combined   cost  for  these  supplies   was  $22,311  per  year.

     Other manpower  needs   that  were not discussed in  the previous processes
included management, vacations and the  laboratory  effort.  A  total of 7,950
man-hours per year were expended in these areas; however,  reductions were made
subsequent to the research project.   The  laboratory manpower  decreased from
4,780  man-hours  to  2,156  man-hours  by reducing  the  various  sampling  and
testing  frequencies.   Management manpower  decreased  from 2,000  man-hours to
600 man-hours.   Because of these  reductions and the reductions  in activated
sludge man-power, the vacation time also decreased from  1,170 man-hours to 717
man-hours.  The scale down  of  the  plant staff  did not affect the plant opera-
tion,  since  the additional manpower was  being directed  toward  the research
effort.  The miscellaneous  manpower requirement following  the research project
decreased from the  original 7,950 man-hours to 3,473 man-hours for an annual
cost of  $19,102 as opposed  tok $42,052 per year.

     The miscellaneous  power cost for  the  plant  was  $5,460  annually.   Power
for the  laboratory,  plant  building and  small  equipment systems are included.
The total operational  cost for the miscellaneous  category, excluding research
associated costs, was  $46,873 per year.

                                     160

-------
 Summary of  Cost  Information

     The UTSD plant was  built  for  a design life  of  20 years.   A summary of the
 total  capital  cost for  the plant  is  shown in Table  41.   Also  shown is  the
 yearly capital  cost for 20  years  at a 6-1/4 percent  interest rate, which  is
 the  bond  interest rate  for the UTSD  plant.   Using  the design  flow for  the
 plant of 5,680 cu m/day  (1.5 mgd)  and  the  yearly  capital cost  of  $263,330,  the
 capital cost for wastewater treatment then became  12.7^/cu  m (48
-------
operation's unit cost  of 18.6 
-------
                                  SECTION 8

                                  REFERENCES

1.  Interim Report for  Research Project,  "An Evaluation of  Pollution Control
    Process, Upper  Thompson Sanitation District,"  prepared by  M &  I,  Inc.,
    Consulting Engineers,  Fort  Collins,  Colorado,  for  EPA MERL Cincinnati,
    Ohio (January 1977).

2.  Hegg, B.A., K.L.  Rakness,  and J.R. Schultz, "A Demonstrated Approach for
    Improving Performance and  Reliability of Biological Wastewater  Treatment
    Plants,"  report   prepared  in  partial   fulfillment   of   EPA   Contract
    No. 68-03-2224, by  M &  I,  Inc.,  Fort  Collins,   Colorado,  for U.S.  EPA,
    Cincinnati, Ohio (1973).

3.  McCarty, P.L., L.  Beck,  and P. St. Amant,  "Biological  Denitrification of
    Wastewater by  Addition  of  Organic Materials.    Proceedings of  the  24th
    Industrial Waste  Conference,  May 6,  7,  and 8,  1969, Lafayette,  Indiana,
    Purdue University (1969).

4.  Process Manual for Nitrogen Control, U.S. Environmental  Protection Agency,
    Technology Transfer Publication (October 1975).

5.  Hill, A.G. and H.T. Spencer, "Mass Transfer in Gas Sparged Ozone Reactor",
    Proceedings of  the  First International  Symposium on Ozone  for Water and
    Wastewater  Treatment  sponsored  by  the  International  Ozone  Institute
    (1975).
6.  Personal  communication  with Mr.  Ed  Opatken,  MERL,  Cincinnati,  Ohio,
    September, 1978.

                                     163

-------





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-------
                                 APPENDIX G

          TABLE G-l.  PROCEDURE FOR OZONE AIR CONCENTRATION TESTING
	AT THE. UPPER THOMPSON SANITATION DISTRICT	

  1.  Set ozonator at desired amperage setting.  Record generator information
      on data sheet (See Table A-2).
  2.  Check Dasibi Meter zero, span and control and sample frequency readings
      and adjust if necessary.
  3.  Prepare wet test chemistry equipment (See Figure A-l).
      a.  Add 400 ml of 2% KI Solution to each of two 500 ml gas washing
          bottles (Note:  Fritted glass diffuser was not used on ozone-air
          inlet tube).
      b.  Connect gas washing bottles in series and connect ozone supply line
          and wet test meter.
      c.  Level wet test meter and adjust water level in the meter.
  4.  Open vent valve and vent test line for two (2) minutes.
  5.  Read and record three consecutive Dasibi Meter readings,
  6.  Set two-way valve to direct ozone-air gas flow to the gas washing
      bottles and open flow control valve to full open (metering valve set for
      2 liters/minute).
  7.  Run approximately 4.5 liters of gas flow through the bottles and record
      field data information on data sheet (See Table A-2).
  8.  Take gas washing bottles to laboratory immediately and have another
      person read and record three more Dasibi Meter readings.
  9.  Quantitatively transfer liquid from gas washing bottles to two separate
      1 liter erlynmeyer flasks.  Rinse tubes and bottles at least three
      times.
 10.  Immediately add 10 ml of 2N Sulfuric Acid (H^SO^.
 11.  Read initial buret volume which contains 0.1N sodium thiosulfate
      solution (^28203).  Note:  Standardize N32S203 using the
      dichromate method.  (Standard Methods Ed. 14, pp. 316).
 12.  Quickly titrate the darker of the 2 flasks to a pale yellow color with
      the Na2S203).
 13.  Add 5 ml starch indicator (See Standard Methods Ed. 14, pp. 317 for
      starch preparation) and  carefully titrate by drop until clear.
 14.  Add 5 ml starch indicator to second flask and again carefully titrate
      dropwise until clear.
 15.  Record final volume buret reading and determine total volume of titrant
      used.  Record on data sheet.
 16.  Complete calculations on data sheet (See Table A-2).

                                     212

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-------
                    TABLE   G-l.    OZONE  PRODUCTION  DATA  RECORDING  SHEET
                                                OZONE SYSTEM PERFORMANCE DATA
                                          OZOHE UTILIZATION AND TRANSFER CALCULATIONS
                                  Date                   ,    Time of Analysis 	
      IKFORMATIOM
     Vrnr Caa;  Plw _ scf»  (25°C) (see graph)
     Wet Tf«t Hctert  Voluae _ L    Temperature
                    Water Vapor Pressure _ in.  H20  (see graph)
LAB IKFORMATIOK
    Ve ! e, .JTtjj C jte tjEC.l  Titratioa _ rals    N of Ha2S203 _ mole eq/L
                   Titratlon . _ mis   N of Na2S203 _ mole eq/L
                                                               Manometer	in.  H20  (suction is negative)
          Concentration In Off Gas:
         Calculate weight of ozone trapped  in KX solution.
             „ - ("L-is-si, (Iltcotlon
                                                                             eq/l)
                                                                                       ml)  (2* IF R3)
                                                                                     —  '  vmole eq '
                      L    '  \**..*.»...MMI ««., ,, mole eq '  ^  gm-ml  '    "•	
         Calculate volume of gas that paaed through wet  test meter.

                 Where:  '  V, • Actual volume L
                           ?2 " Standard Pressure -  406.8 in H20
                           P, » Adjusted Pressure "(Plant Atmospheric Pressure  (7460) of, 314 in. H20)
                                              - (water vapor pressure) + (wet test manometer pressure - Note:
                               negative).     PI -	-	+	          in. H20
                           T2 - Standard Temperature (absolute)  - 77°F + 459.6  - 536.6°R
                           Tj - Actual Temperature (absolute) 	°F -  459.6 =        °R
         Calculate ozone concentration in off gas.
                                   C-
                                           T>
             pp«/vol - ( _ vg/L air)  (1,000,000)
             Qzoil^ Cengfflntration;
                                                                  ppm/vol  (25°C)
         Calculate weight of ozone trapped in KI solution.

         Calculate Residual Ozone Concentration.
                                IS) <-
        mg/L H20 - (__
PapqjLJ^at in VffiQCi
     Calculate ozone lost in vent.
        lb»/d«y - (	ft3/min
R«*idual OEQBC!
                                                g/L air) (28.32 L/ft3)
                                                                                  (1440 min/d.y)
         Calculate aaount of residual ozone in the water.
             ib.rtay - C	«S/L H20) (	mgd) (8.34 lbs/8al) - .
        tt Transfer:
                                                                       _lbs/day
         Percent Clone Transfer -  Cozone supply rate (Ibs/day) - ozone lost in vent (lbs/dav»  (100)
                                                ozone supply rate (Ibs/day)
                                                          _(lbs/day)  (100)
                                                 _(Ibs/day)
     Effceetvg Ozoqe Dosage;
                                                          _mg/L H20
                                                                                                           Ibs/day
         Concentration of Effective Ozone Dosage - (Percent Transfer efficiency) (applied ozone dosage) - (	%)  (	mg/L H 0)
                                                                                        (Continued)
                                                           214

-------
  TABLE  G-2   (CONT).    OZONE  PRODUCTION DATA  RECORDING  SHEET
OZONE SYSTEM PERFORMANCE DATA

GENERATOR OUTPUT, APPLIED OZONE DOSAGE,'' DISINFECTION RESULTS, POWER REQUIREMENTS  (Continued)
        Calculate Ozone supply rate.
        Ibs/day - (	

Applied Ozone Dosage;

        mg/L H20 - (_
                             ftVmin) ( _ mg/L alt)  (28.32 l/ft') t^^o Tjf' <144° -^/^^
                             Its/day) (—
DISINFECTION RESULTS

    Values expressed in number of coliforms/100 ol
                                                    OTN
                               Total

                               Fecal
                                                                   1ft V
                                                                 0, Basin
                                                                 Effluent
                                                                                            _lbs/day
     Calculate Power Utilization
                                    p
                                   (^2.) (4.8 watts/sec) 
-------
                                 APPENDIX H
          TABLE H-l.  PROCEDURE FOR CONTACT BASIN OFF GAS TESTING
                      AT THE UPPER THOMPSON SANITATION DISTRICT	

 1.  Prepare wet test chemistry equipment (See Figure B-l).
     a.  Add 400 ml of 2% KI solution to one gas washing bottle.
     b.  Connect wash bottle to test line and wet test meter.
     c.  Connect vacuum line to wet test meter vent.
     d.  Level wet test meter and adjust water level in the meter.
     e.  Open vacuum valve until moderate gas flow rate is established.
 2.  Run approximately 12 liters of gas through the botle and record field
     information on data sheet (See Table B-2).
 3.  Take gas washing bottle to laboratory immediately.
 4.  Quantitatively transfer liquid from gas washing bottle to a 1 liter
     Erlenmyer flask.  Rinse tube and bottle at least 3 times.
 5.  Immediately add 10 ml of 2N Sulfuric Acid (H2S04).
 6.  Read initial volume of buret which has been filled with 0.1N sodium
     thosulfate solution (^28203).  Note:  Standardize Na2S203
     using the dichromate method.  (Standard Methods Ed. 14, pp. 316).
 7.  Quickly titrate to pale yellow with ^28203.
 8.  Add 5 ml starch indicator (See Standard Methods - Edition 14, pp. 317
     for starch preparation) and slowly titrate by drop to a clear end
     point.
 9.  Record final volume of buret and determine total volume titrant used.
     Record information on data sheets (See Table B-2).
10.  Complete calculations on data sheet (See Table B-2).
                                    216

-------
                                                      60
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-------
                  TABLE   H-2.     OZONE  OFF-GAS  DATA  RECORDING  SHEET
                                                  OZONE SYSTEM PERFORMANCE DATA
                          GENERATOR OUTPUT, APPLIED OZONE DOSAGE, DISINFECTION RESULTS, POWER REQUIREMENTS
                                 Date	    Time of Analysis 	
rtna TKTCP.KATIOT
     Ceaeratort  No.
                               Voltage
                                             _volts    Amperage _
     Catjrgolert  Exchanger Temperature
                 Separator Pressure
     Air Co»prapjor;  Seal Water Pressure
     A_lr Pratcgataentt  Voluae	cfa
     Pattbj HaCert Reading 	
     W«t Teat Hetcrt  Volume
                                                  Inlet Temperature _
                                                                    _amps    Controller Setting
                         isig    Temperature _
ipm/vol    Corrected Reading	ppm/vol
                                 _L    Temperature	F    Man
                    Water Vapor Pressure	In. H20 (see graph)
    Heating Toueri  On 	   Off 	  Refrigeration;   On
                                                                           Off
 Main Pressure	pslg



	°F    Dewpolnt (	°c)


_in. H20 (suction  Is negative)
                                                                                                      Left
                   System Amperage
                   Watt-Hour Hater - Revolutions
    Wat Test Kagar;  Titration
                                       sis   N of
                                                  Na2S2°3 -
                                                               Leg 1  Amperage _
                                                               Leg 2  Amperage _
                                                               Leg 3  Amperage _
                                                             Time	sec.
                                                                 _ mole eq/L
         QOTPUT AM LAPPLIED 020KE DOSAGE CALCULATIONS
         Calculate Height of ozone trapped in KI Solution.
                              (Tltratlm
                                                            DASIBI  INFORMATION
                                                             Span 	
                                                            Inlet Temp. 	°F
                                                            Meter Readings:
             Wt- (-
                             L   ' ^	•*"•' vmole eq'  *•  gm-ml
         Calculate voluae of gas that passed through wet  test meter.
                                                      in. H20J
                  Where t    Vj - Actual voluae in L
                           P2 - Standard Pressure - 406.8 in. H20
                           P! - Adjusted Pressure - (Plant Atmospheric Pressure (7460) of 3X4 in. H20)
                                                                                                                   Right f
                                               - (water vapor pressure)  + (wet test manometer pressure - Note:  suction is
                               negative).
                          T2 - Standard temperature (absolute) - 77°F + 459.6 - 536.6°R
                          Tj • Actual Temperature (absolute) -	°F + 459.6  -	
         Calculate ozone concentration.
             •S/L air - (        ag) (	j-) -	mg/L air
             pp«/vol - (	r-rrr*8) (1,000,000) (-J—-) - 	ppn/vol (25°C)
         Calculate ozonated air flow rate.
                  Where:   V^ - Actual Volume in Ft3
                                                                                                       _scfm (25°C)
                          P2 • Standard Pressure (absolute) - Gauge Pressure-*- Atmospheric Pressure = 6 psig + 14.7 psi - 20.7  psla
                          P! - Actual Pressure (absolute) ~ Gauge  Reading (pslg) 4- Plant Atmospheric pressure  (7460)  of 11.34 psi o
                                                                       ) x 0.036 psi/in.

                          T2 " Standard Teaperature for Rotameter  (absolute) - 70°F + 459.6 - 529. 6°R
                                                                                 °F + 459.6 - _
                             • Actual Tetaperature for Rotaneter (absolute) - _
                             - Standard Temperature of 25°C (absolute) » 77°F + 459.6 » 536. 6°R
                                                                                                 (Continued)
                                                           218

-------
TABLE  H-2  (CONT) •..   OZONE  OFF-GAS DATA  RECORDING . SHEET
OZOHE SYSTEM PERFORMANCE DATA
                    14
                                         MATER VAPOR PRESSURE
                                               VK
                                            TEMPERATURE
                |,
                    10
                                       55       60      65      70
                                         WET TEST METER TEMP. (°F)
                                                                        75
                                                                                80
                                             OFF GAS FLOW BATE
                               OZONE ROOM EXHAUST COVERED, SCUM CAPS ON, OUTFALL SUBMERGED
195
190
185
180
175
170
165
160
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20 30 40 50 60 70 80 90
                                        GENERATOR FLOW-scfm (25°C)
                          © ACTUAL TESTS
                                               219

-------
                                    TECHNICAL REPORT DATA
                             (Please read Instructions on the reverse before completing)
  1, REPORT NO,
  EPA-600/2-80-016
                   3. RECIPIENT'S ACCESSION-NO.
  4. TITLE AND SUBTITLE

  EVALUATION OF POLLUTION CONTROL PROCESSES
  Upper Thompson  Sanitation District
                   5. REPORT DATE
                     June 1980  (Issuing  Date)
                   6. PERFORMING ORGANIZATION CODE
  7. AUTHORtS)        ~~                                ~~
     Bob A. Hegg, Kervin  L.  Rakness, Larry D. DeMers,
     and Bobert H. Cheney
                   8. PERFORMING ORGANIZATION REPORT NO.
    JRFORMING ORGANIZATION NAME AND ADDRESS
     Upper Thompson Sanitation District
     P.O. Box 568
     Estes Park, Colorado   80517
                   10. PROGRAM ELEMENT NO.
                   A35B1C  SOS #3  Task C/09
                   11. CONTRACT/GRANT NO.

                      Grant R-803831
 12. SPONSORING AGENCY NAME AND ADDRESS
 Municipal Environmental  Research Laboratory—Gin.,OH
 Office of Research and Development
 U.S.  Environmental Protection Agency
 Cincinnati, Ohio  45268
                   13. TYPE OF REPORT AND PERIOD COVERED
                     5/76-9/79  Final
                   14. SPONSORING AGENCY CODE
                    EPA/600/14
 15. SUPPLEMENTARY NOTES

     Edwin F.  Earth - Project  Officer
(513) 684-7641
  P  4,4,.       Upper ThomPson Sanitation District  (UTSD)  advanced wastewater  treatment
  facility, located in Estes Park, Colorado, incorporated  several unique unit  processes.
  Among these were flow  equalization, attached growth nitrification, mixed media filtra-
  tion and ozone disinfection.   Plant design flow was 5,680 cu m/day (1.5 mgd  to 1.0 ragd
  The activated sludge,  nitrification and filtration  processes have two parallel trains
  By selectively using one  half of the available units design flow conditions  were
  achieved at one-half the  plant design flow rate.
       Overall plant performance in terms of BOD5 and TSS  removal was consistent,
  averaging 95 percent and  96  percent, respectively.   Ammonia oxidation was not  as  con-
  sistent, due to loading extremes and cold weather operating conditions.  Performance
  characteristics of two nitrification tower media types (plastic dumped and redwood
  slats)  were different.
       The air-fed ozone disinfection system was operated  intermittently because of
  required modifications.   Special studies were conducted  to determine performance
  information.   When operating,  good disinfection performance was achieved.
 17.
                                KEY WORDS AND DOCUMENT ANALYSIS
                  DESCRIPTORS
                                              b.lDENTIFIERS/OPEN ENDED TERMS
                                                                         c. COSATI Field/Group
 Wastewater*
 Nitrogen cycle*
 Activated sludge process
 Electric power demand
 Disinfection
     Attached  growth
     Ozone  disinfection*
     Nitrification
     Denitrification
       13B
   IISTRIBUTION STATEMENT

    Release  to Public
     19. SECURITY CLASS (ThisReport)'
       None
21. NO. OF PAGES
      234
                                              20. SECURITY CLASS (Thispage)
                                                None
                               22. PRICE
EPA Farm 2220*1 (9-731
                                            220
                                                                   ft U.S. GOVERNMENT PBINTINQ OFFICE: 1980 -657-146/5698

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