FINE PORE DIFFUSER SYSTEM EVALUATION FOR THE
 GREEN BAY METROPOLITAN SEWERAGE DISTRICT
                       by

                  James J. Marx
       Rusk Environment and Infrastructure, Inc.
        (formerly Donohue and Associates, Inc.)
            Sheboygan, Wisconsin 53083
        Cooperative Agreement No. CR812167
                 Project Officer

               Richard C. Brenner
Water and Hazardous Waste Treatment Research Division
       Risk Reduction Engineering Laboratory
              Cincinnati, Ohio  45268
 RISK REDUCTION ENGINEERING LABORATORY
   OFFICE OF RESEARCH AND DEVELOPMENT

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                                  DISCLAIMER
   Development of the information in this report has been funded in part by the U S
Envoynmenta  Protection Agency under Cooperative Agreement No. CR812167 L the
American Society of Civil Engineers.  The report has been subjected to Agency p^r and
administrative review and approved for publication as an EPA document  Mentfonof trad
names; or commercial products does not constitute endorsement or recoimnenda on ?or™

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                                     FOREWORD
    Today's rapidly developing and changing technologies and industrial products and
 practices frequently carry with them the increased generation of materials that, if
 improperly dealt with, can threaten both public health and the environment The U S
 Environmental Protection Agency (EPA) is charged by Congress with protecting the' "
 Nation s land, air, and water resources. Under a mandate of national environmental laws,
 the Agency strives to
 formulae and implement actions leading to a compatible balance between human activities
 and the ability of natural systems to support and nurture life.  These laws direct EPA to
 perform research to define our environmental problems, measure the impacts, and search
 for solutions.                                                                ^«»vu

    The Risk Reduction Engineering Laboratory is responsible for planning, implementing
 and managing research, development, and demonstration programs to provide an
 authoritative, defensible engineering basis in support of the policies, programs, and
 regulations of EPA with respect to drinking water, wastewater, pesticides, toxic substances,
 solid and hazardous wastes, and Superfund-related activities.  This publication is one of the
 products of that research and provides a vital communication link between the researcher
 and the user community.

    As part of these activities, an  EPA cooperative agreement was awarded to the American
 Society of Civil Engineers (ASCE) in 1985 to evaluate the existing data base on fine pore
 diffused aeration systems  in both  clean and process waters, conduct field studies at a
 number of municipal wastewater treatment facilities employing fine pore aeration and
 prepare a comprehensive design manual on the subject This manual, entitled "Design
 Manual -Fine Pore Aeration Systems," was completed in September 1989 and is available
 hrough EPA'sCenter for Environmental Research Information, Cincinnati, Ohio 45268
 IcA   P°rt N?' EPA/625"1-89/<>23). The field studies, carried out as contracts under the
 AbCE cooperative agreement, were designed to produce reliable information on the
 perforMance and operational requirements of fine pore devices under process conditions
 fhese studies resulted in 16 separate contractor reports and provided critical input to the
design manual.  This report summarizes the results of one of the 16 field studies.


                                     E. Timothy Oppelt, Director
                                     Risk Reduction Engineering Laboratory
                                          ui

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                                     PREFACE
    In 1985, the U.S. Environmental Protection Agency funded Cooperative Research
 Agreement CR812167 with the American Society of Civil Engineers to evaluate the existing
 data base on fine pore diffused aeration systems in both clean and process waters, conduct
 field studies at a number of municipal wastewater treatment facilities employing fine pore
 diffused aeration, and prepare a comprehensive design manual on the subject This manual,
 entitled "Design Manual - Fine Pore Aeration Systems," was published in September 1989
 (EPA Report No. EPA/725/1-89/023) and is available from the EPA Center for
 Environmental Research Information, Cincinnati, OH 45268.

    As part of this project, contracts were awarded under the  cooperative research
 agreement to conduct 16 field studies to provide technical input to the Design Manual. Each
 of these field studies resulted in a contractor report. In addition to quality assurance/quality
 control (QA/QC) data that may be included in these reports, comprehensive QA/QC
 information is contained in the Design Manual. A listing of these reports is presented below.
 All of the reports are available from the National Technical Information Service, 5285 Port
 Royal Road, Springfield, VA 22161 (Telephone: 703-487-4650).

 1.     "Fine Pore Diffuser System Evaluation for the Green Bay Metropolitan Sewerage
       District" (EPA/600/R-94/093) by J J. Marx

 2.     "Oxygen Transfer Efficiency Surveys at the Jones Island Treatment Plants, 1985-
       1988" (EPA/600/R-94/094) by R. Warriner

 3.     "Fine Pore Diffuser Fouling:  The Los Angeles Studies" (EPA/600/R-94/095) by M.K.
       Stenstrom  and G. Masutani

 4.     "Oxygen Transfer Studies at the Madison Metropolitan Sewerage District Facilities"
       (EPA/600/R-94/096) by W.C. Boyle, A. Craven, W. Danley, and M. Rieth

 5.     "Long Term Performance Characteristics of Fine Pore  Ceramic Diffusers at Monroe,
       Wisconsin" (EPA/600/R-94/097) by D.T. Redmon, L. Ewing, H. Melcer, and G.V.
       Ellefson

 6.     "Case History of Fine Pore Diffuser Retrofit at Ridgewood, New Jersey"
       (EPA/600/R-94/098) by J.A. Mueller and P.D. Saurer

7,     "Oxygen Transfer Efficiency Surveys at the South Shore Wastewater Treatment
       Plant,  1985-1987" (EPA/600/R-94/099) by R. Warriner


                                         iv

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 8.     "Fine Pore Diffuser Case History for Frankenmuth, Michigan" (EPA/tfOO/R-94/100)
       by T.A. AHbaugh and S J. Kang

 9.     "Off-gas Analysis Results and Fine Pore Retrofit Information for Glastonbury,
       Connecticut" (EPA/600/R-94/101) by R.G. Gilbert and R.C. Sullivan

 10.    "Off-Gas Analysis Results and Fine Pore Retrofit Case History for Hartford,
       Connecticut" (EPA/600/R-94/105) by R.G. Gilbert and R.C. Sullivan

 11.    "The Measurement and Control of Fouling in Fine Pore Diffuser Systems"
       (EPA/600/R-94/102) by E.L. Barnhart and M. Collins

 12.    "Fouling of Fine Pore Diffused Aerators: An Interplant Comparison"
       (EPA/600/R-94/103) by C.R. Bafflod and K. Hopkins

 13.    "Case History Report on Milwaukee Ceramic Plate Aeration Facilities"
       (EPA/600/R-94/106) by L.A. Ernest

 14.    "Survey and Evaluation of Porous Polyethylene Media Fine Bubble Tube and Disk
       Aerators" (EPA/600/R-94/104) by  D.H. Houck

15.    "Investigations into Biofouling Phenomena in Fine Pore Aeration Devices"
       (EPA/600/R-94/107) by W. Jansen, J.W. Costerton, and H. Melcer

16.    "Characterization of Clean and Fouled Perforated Membrane Diffusers"
       (EPA/600/R-94/108) by Ewing Engineering Co.

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                                     ABSTRACT


    The Green Bay Metropolitan Sewerage District retrofitted two quadrants of their
activated sludge aeration system with ceramic and membrane fine pore diffusers to provide
savings in energy usage compared to the sparged turbine aerators originally installed
Because significant diffuser fouling was expected, the two diffuser types were closely
monitored over an 18-month period.  The oxygen transfer efficiencies of the full-scale
systems were measured using off-gas techniques. The effects of diffuser fouling and the
effectiveness of cleaning procedures were evaluated in the laboratory using dynamic wet
pressure and steady-state clean water oxygen transfer tests. Although fouling was
significant on both types of diffusers, cost-effective cleaning procedures were developed  The
ceramic disc diffusers provided better long-term performance than the membrane tube
diffusers, which irreversibly lost oxygen transfer efficiency with time in use. Collectively
the fine pore diffuser systems provided a 30% savings in electrical power usage compared to
the original sparged turbine aerators.

    This report was submitted in partial fulfillment of Cooperative Agreement No.
CR812167 by the American Society of Civil Engineers under subcontract to Rusk
Environment and Infrastructure, Inc. (formerly Donohue and Associates, Inc.) under the
partial sponsorship of the U.S. Environmental Protection Agency.  The work reported herein
was conducted over the period of 1986-1987.
                                         VI

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                                    CONTENTS


 Foreword	
 D  f	111
 Preface  	
                       • •••....... ••••••••»••«•-•••••••••.........,.,,.  |y
 Abstract	
 _,.                       	vi
 Figures  	
 Tables	       	V!"
                          	u

 Introduction	   .                        1
 Description of Facilities  	      	  2
 Study Methods	             	  „
    Oxygen Transfer Efficiency	.....'  	  R
    Diffuser Evaluation .	       	     11
    Foulant Analysis	                   	  •-
 Results and Discussion	. . .	        	  13
    Operational Procedures and Goals	  13
    Oxygen Transfer Efficiency Versus Time	\	  15
      Off-Gas Testing	  15
      Efficiency Factor	             	  ^n
    Oxygen Transfer Efficiency Versus Air Flow Rate	     22
    Apparent Alpha Versus Time                                      	  23
    Pilot Diffuser Evaluations	                                      3n
      Summer 1986	" " "	'	  ,"
      October 1986  	'.'.'.'.'.'.'.'.'.	 34
      November 1987	   	   35
    Grid Diffuser Evaluations		
      November 1986	                ,	 41
      July 198?	;;;;;;;;;;;;;;;;; ;;;;;;;;;;;;;;;;;;; 45
    Foulant Analysis	         	 --
    Cost Analysis	               	 „
      Capital	 s_
      Operation	         	 __
      Maintenance	           '	 ^
      Summary	               	 ,_
Conclusions	          '	
Recommendations	            	 ,_
References	            	 ,q
Appendices

    A. Efficiency  Factor Calculation Description	            70
    B. Statistical Review of the Off-Gas Test Results	      73
    C. Operational  Cost Data Summaries	' ] * ]	  98

                                       vit

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                                      FIGURES
Number
 1  Schematic of the Green Bay Wastewater Plant	 3
 2  Aeration Basin Zones and Grids  	 5
 3  Hood Positions Used for Off-Gas Testing	              9
 4  Oxygen Transfer Efficiency (Off-Gas Method) Versus Time  . . .	  17
 5  Contact Basin Efficiency Factor Versus Time	  21
 6  Oxygen Transfer Efficiency Versus Position and Air Flow
    Rate - Contact Basin Ceramic Diffusers Before Cleaning		  24
 7  Oxygen Transfer Efficiency Versus Position and Air Flow
    Rate - Contact Basin Ceramic Diffusers After Cleaning	  25
 8  Oxygen Transfer Efficiency Versus Position and Air Flow
    Rate - Contact Basin Membrane Diffusers Before Cleaning	  26
 9  Oxygen Transfer Efficiency Versus Position and Air Flow
    Rate - Contact Basin Membrane Diffusers After Cleaning	  27
 10 Oxygen Transfer Efficiency Versus Position and Air Flow
    Rate - Reaeration Basin Ceramic Diffusers Before
    Cleaning	  -     23
 11 Oxygen Transfer Efficiency Versus Position and Air Flow
    Rate - Reaeration Basin Membrane Diffusers Before
    Cleaning	                29
 12 Photographs of Fractured Ceramic Diffusers	  39
 13 Ceramic Diffusers Test Results - Grid Units Removed
    November 1986	                    42
 14 Membrane Diffusers Test Results - Grid Units Removed
    November 1986	  44
 15 Ceramic Diffusers Test Results - Grid Units Removed July
    19»7	  46
 16 Membrane Diffusers Test Results - Grid Units Removed July
    1987	  48
 17 Photographic Comparison - New Versus Hose-Brush-Hose
    Cleaned Contact Basin Membrane Diffuser	  49
 18 Photographic Comparison - New Versus Hose-Flush-Hose
    Cleaned Contact Basin Membrane Diffuser 	 50
 19 Photographic Comparison - New Versus Hose-Brush-Hose
    Cleaned Reaeration Basin Membrane Diffuser	 51
20 Photograph of Foulant From Contact Basin Ceramic Diffuser	 53
21 Power Cost Versus Time	m            61
                                        Vlll

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                                      TABLES
 Number                                                                      Page

 1   Fine Pore Aeration System Design Criteria	. .  4
 2   Fine Pore Diffuser Configuration Summary	  6
 3   Clean Water Oxygen Transfer Test Results	  7
 4   Diffuser Preventive Maintenance Summary	  14
 5   Operating Data for May 1986 - October 1987	]', ' '  15
 6   Statistical Analysis of Alpha'-SOTE Data	  18
 7   Variable Air Flow Rate Testing - May 14, 1986	  23
 8   Apparent Alpha as a Function of Time in Service	  30
 9   Diffuser Characterization Results - New Membrane Discs	  31
 10  Diffuser Characterization Results - New Membrane Tubes	  32
 11  Ceramic Diffuser Test Results - Pilot Units Removed
    June 11, 1986 	              32
 12  Ceramic Diffuser Test Results - Pilot Units Removed
    June 22, 1986 	. . . -	  33
 13  Ceramic Diffuser Test Results - Pilot Units Removed
    October 21, 1986	  35
 14  Membrane Diffuser Test Results - Pilot Units Removed
    October 28, 1986	  36
 15  Final Characterization of Used Ceramic Diffusers	  37
 16  Final Characterization of Used membrane Diffusers	  40
 17  Comparison of New and Used Membranes	  52
 18  Ceramic Diffuser Foulant Analyses Summary	  55
 19  Membrane Diffuser Foulant Analyses Summary	  56
20  Summary of Capital Costs	        58
21  Electrical Power Usage and Cost Summary	  50
22  Estimated Maintenance Costs	  53
23  Alternative Aeration Systems Cost Summary	  55
                                        IX

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INTRODUCTION
             The Green Bay Metropolitan Sewerage District (GBMSD) operates an
             activated sludge secondary treatment facility. Historically, about half of
             the plant's total electrical energy needs were for operating the sparged
             turbine aeration system. In the spring of 1983, Donohue & Associates
             was retained to prepare a Predesign and Feasibility Report for Aeration
             System Modifications.1 The report published in December  1983 was
             supported by field testing conducted during the summer of 1983. Of the
             alternatives studied, fine pore ceramic diffusers showed  potential for
             significant energy savings. However, a major concern with  the fine pore
             diffusers was fouling and the effects that fouling could have on the overall
             system economics by increasing operating pressure, decreasing oxygen
             transfer  efficiency and increasing maintenance costs  for diffuser
             cleaning.

             Because of the concern over fouling, the report recommended that fine
             pore diffused air aeration be tested by installing a full-scale ceramic
             diffuser system in one quadrant of the aeration complex. Since the 1983
             field tests showed that a substantial portion of the foulant materials was
             soluble in acid, the recommended ceramic system was to include an in
             situ acid gas injection system. Preliminary calculations presented in
             Appendix B to the 1983 Report showed that to operate the fine pore
             system in a mode equivalent to the design year loadings, approximately
             40 percent of the influent flow would  have to be fed to the fine pore
             system and 60 percent to one or more of the sparged turbine systems.

             In the fall of 1984, Donohue was asked to evaluate the Wyss Flex-A-Tube
             membrane diffuser as an alternate fine pore system. The manufacturer
             claimed that the flexible membrane tube diffusers normally did not foul
             and, if fouling occurred, it could be controlled by flexing the units. A
             letter report dated November 30, 1984 concluded that the flexible
             membrane diffuser system would also be worth evaluating in a full-scale
             test. Based on the data available at the time, the ceramic diffusers were
             expected to have a higher oxygen transfer efficiency than the membrane
             diffusers when  the  systems were clean. However, since fouling was
             expected to adversely affect the oxygen transfer efficiency, the flexible
             membrane units could have produced better oxygen transfer efficiency
             in the long run if in fact the diffusers did not foul.

             Because the cost effectiveness of ceramic disc and flexible membrane
             tube diffusers was believed to be similar, and the fouling characteristics
             and maintenance procedures were potentially different, it was decided
             to install and test both types of fine pore diffusers. Testing two fine pore
             diffuser systems also provided the opportunity to try to treat all of the

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             wastewater through the test quadrants and achieve substantial energy
             savings during the test period.                           !
DESCRIPTION OF FACILITIES
             The GBMSD activated sludge facility treats a mixture of metropolitan
             (Metro),  and pulp and paper mill (mill) wastewaters. The Metro
             wastewaters comprise municipal and industrial wastes including  a
             seasonal contribution from vegetable canning industries. The Metro
             wastewaters receive preliminary and primary treatment before entering
             the  activated sludge system. The mill wastewaters receive primary
             treatment at the mills before they enter the plant through separate
             interceptor  sewers and are pumped  directly to the activated sludge
             system. Plant recycle streams which include decant liquor from a Zimpro
             sludge heat treatment process are returned  to the primary effluent
             channels.

             The activated sludge process is a contact stabilization system consisting
             of four quadrants (Figure 1). Each quadrant includes a 73.3 feet by 244
             feet by 20.5 feet water depth contact basin and a 36.3 feet by 244 feet by
             22.5 feet water depth reaeration basin. Each contact basin was originally
             equipped with twelve 125 HP sparged turbine aerators. The reaeration
             basins had six 75 HP aerators. The process air is supplied by four 2500
             HP centifugal compressors each having a capacity of 44,500 scfm at a
             discharge pressure of 12 psig.

             Quadrant number 2 was retrofitted with ceramic disc diffusers while
             quadrant number 4 received the flexible membrane tube diffusers. The
             design criteria for selecting the number and distribution of fine pore
             diffusers in  the aeration basins are presented in Table 1. The design
             criteria were based on the results of the field studies conducted in 1983,
             operating experience  with the sparged  turbines, and information
             supplied by  the manufacturers of the fine pore  aeration systems.  The
             alpha values used for design, 0.68 in the contact basins and 0.90 in the
             reaeration basins, were selected based on the results of the  1983 field
             work and with consideration given to other design constraints such as
             maximizing  the power savings during the test period by treating the
             entire plant flow through the two fine pore diffuser equipped quadrants.
             However, this design strategy was only viable if the actual alpha values
             were equal to or greater than the values used for design. In the event that
             alpha was lower or plant loadings were higher than expected, additional
             aeration capacity could be added by placing one or more of the sparged
             turbine systems in service.

             The contact basins were divided into three zones and subdivided into ten
             grids. The number of diffusers per grid was the highest in the tank inlet

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            Table 1 • Fine Pore Aeration System Design Criteria
            Biochemical Oxygen Demand (BODs)1
               Average Day (50th Percentile)
               Maximum Month
               Maximum Day (99th Percentile)
                              *y
            Oxygen Requirement

            Contact Basins
               Size
               Number
               Oxygen Demand
               Oxygen Demand Profile Zone 1
                                    Zone 2
                                    ZoneS
               Alpha
               Beta
               Diffuser Submergence

            Reaeration Basins
               Size
               Number
               Volume
               Oxygen Demand
               Oxygen Demand Profile
               Alpha
               Beta
               Diffuser Submergence
 161,000 Ib/day
 202,000 Ib/day
 239,000 Ib/day

 1.0 O2/lb BODs applied
733' x 244' x20.5' deep
4
75% of quadrant total
55%
30%
15%
0.60-0.75
0.95
19.1 feet
363'x 244'x 22.5'deep
4
1.5 xlO6 gal each
25% of Quadrant Total
Uniformly Distributed
0.90
0.95
19.1 feet
            1 Calculated from data reported for January 1982 through April 1983. A total of 478
            values were used.
             Based on 1983 off-gas results.
           zone and lowest in the tank outlet zone. The reaeration basins were
           divided into six grids. Since the oxygen demand was expected to be
           relatively uniform, the number of diffusers per grid was constant The
           layout of the aeration zones and grids are shown in Figure 2.

           The number of diffusers installed in each grid and the design air flow
           rates per diffuser are summarized in Table 2. The design average air flow
           rates used for the ceramic diffusers, 2.1 scfm/unit in the contact basin
           and 1.9 scfm/unit in the reaeration basin, were relatively high compared
           to normal practice of designing for about 1.25 scfm/unit. The high air
           rates in the contact basin resulted from providing the maximum number
           of diffusers that would physically fit in the basin inlet grids and then using

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  Reaeration
   Basin 4
 Contact
 Basin 4
Contact
Basin 2
Reaeration
 Basin 2
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            Mil! Waste
Pilot Headers — * —
                                             FIGURE 2
                                             Aeration Basin Zones and Grids

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Table 2 - Fine Pore Diffuser Configuration Summary
No. of Diffusers Diffusers Diffuser
Zone Grids jerGrid per Zone Density1
Contact Basin No. 2 - Ceramic Disc Diffusers
1 4 805 3220 0.54
2 4 490 1960 033
3 2 474 948 0.16
Basin Total 6128
Reaeration Basin No. 2 Ceramic Disc Diffusers
1 6 358 2148 0.24
Contact Basin No. 4 - Membrane Tube Diffusers
1 4 616 2464 0.41
2 4 350 1400 0.23
3 2 378 756 0.13
Basin Total 4620
Reaeration Basin No. 4 - Membrane Tube Diffusers
1 6 233 1398 0.16
Density = diffusers per square foot of floor area
Design
Air Rate
scfm/unit
2.1
2.1
2.1
1.9
2.9
2.9
2.9
2.6
the same diffuser air rate for all the grids in the basin. The higher diffuser
air flow rates at design average loadings normally would not be used
because the higher oxygen transfer rate required to handle the peak
diurnal variations in organic loading would have to be achieved at
diffuser air flow rates outside the most efficient range of operation. It
was possible in this application because the  mill wastes provided
relatively constant diurnal loadings.

If the number of diffusers had not been constrained by space, more
diffusers could have been provided for a minimal increase in the capital
cost. If the design average diffuser air flow rate had been 1.25 scfm/unit
rather than 1.9 scfm/unit, the clean water oxygen transfer efficiency
would have been 6 to 8 percent higher.

The membrane system was designed for an air flow rate per diffuser of
2.9 scfm per unit in the contact basin and 2.6 scfm per  unit in the
reaeration basin. The manufacturer's recommended design range for the
tube diffusers was between 2.0 and 5.0 scfm per unit

Before the aeration equipment was approved for manufacture, shop tests
were conducted to determine the clean water oxygen transfer efficiency.
The tests were  conducted in accordance with the ASCE Standard

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            procedure and witnessed by Jim Marx of Donohue & Associates and
            Mike Pierner of the GBMSD. The Sanitaire system was tested at their
            test facilities in Glendale, WI.2The tests were conducted in a 34.3-foot
            by 6- foot rectangular tank. The Parkson system was tested by Gerry Shell
            Environmental Engineers in a 21-foot diameter test tank. The results
            of the clean water tests are summarized in Table 3.

            The Sanitaire aeration  system met the specified oxygen transfer
            efficiencies. The Parkson diffusers performed substantially better than
            the specified standard oxygen transfer efficiency (SOTE) of 27.5 percent.
            Since the number of diffusers was not reduced to account for the higher
            SOTE, the projected design air flow rates per membrane diffuser were
            reduced to about 2.0 scfm/unit in the reaeration basin and 2.5 scfm/unit
            in the contact basin.

            In addition to installing the fine pore diffusers, inlet flumes were built in
            the contact basins to distribute the incoming wastewater across the entire
            width of the basins.  The flumes were deemed necessary because
            grid-type diffuser systems are considered by many to provide poor lateral
            mixing. The 4'-6" wide by 7'-10" deep flumes have two rows of one-foot
            diameter holes on 2'-0" centers in the floor. The number and^ize of the
            holes were selected to provide several inches of headloss. No holes were
Table 3 - Clean Water Oxygen Transfer Test Results
Zone
            Specified Air Flow Rate    Diffuser
            	(scfm)	   Density
            /1000 cu ft   /diffuser      sq ft/unit
                                                  SOTE
Specified
 SOTE1
Sanitaire Ceramic Discs - Contact Basin
1           57.3          2.2           1.9
2           32.4          2.1           3.2
3           16.2          2.1           6.4
            Mean Weighted Average2
Sanitaire Ceramic Discs - Reaeration Basin
All         21.8          1.9           4.3
Parkson Membrane Tubes - Contact Basin
1           59.9          2.9           2.4
2           34.4          2.9           4.2
3           183          2.9           7.9
            Mean Weighted Average2
Parkson Membrane Tubes - Reaeration Basin
All         20.8          2.6           6.3
                                                  31.0
                                                  35.7
                                                  38.3
                                                  33.6

                                                  36.2

                                                  31.4
                                                  33.8
                                                  31.7
                                                  32.2

                                                  34.9
26.8
35.4
31.9
30.2

34.6

27.5
275
27.5
275

27.5
 Standard oxygen transfer efficiency, i.e., clean water at 20°C, barometric pressure of 29.92 in. hg and
zero dissolved oxygen.
 Weighted by the air flow rate to the grid.

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            provided at the center of the flume where the mixed liquor enters
            through a single large opening.

            Five removable pilot headers were provided in each contact basin and
            two  were provided in  each reaeration basin so  diffusers could be
            obtained for visual observation and testing without having to drain the
            basins. Each removable header was equipped with four diffusers at a
            submergence of about 17 feet The headers were  placed at the inlet,
            middle and outlet of the contact basins and at the inlet and outlet of the
            reaeration basins (Figure 2). The diffusers on the removable headers and
            two  diffusers per fixed grid were  provided  with pressure taps for
            monitoring pressure drop across the diffuser elements, also known as
            dynamic wet pressure (DWP).

            A two-stage in-line air filter was provided on the main header to the
            ceramic disc quadrant. The air filter was originally designed to remove
            more than 99.9 percent of  all particles greater than or equal to 0.3
            microns in size. After startup, problems were encountered with excessive
            headless across the filter so the second stage elements were changed to
            a coarser medium. The filtration efficiency of the modified filter was 98
            percent of all particles greater than or equal to 1.0 micron.

            The centrifugal compressors did not require modification because the
            12 psig discharge pressure  was  more than adequate for the 19-foot
            diffuser submergence provided.
STUDY METHODS
             Oxygen Transfer Efficiency

             The oxygen transfer performance of the two fine pore aeration systems
             was evaluated by conducting tests on the full-scale systems using the
             off-gas method.4 The off-gas tests  were conducted by the Ewing
             Engineering Company (Milwaukee, Wisconsin). A typical off-gas test
             was conducted in two days. One day was used to survey 24 positions in
             each of the contact basins. The second day was used to survey 12 positions
             in each of the reaeration basins. The sampling positions are shown in
             Figure 3. So that data from the two systems would be comparable, several
             sampling hoods were used and the analyzer was moved in a serpentine
             pattern starting at the inlet of one basin and moving across to the second
             basin before moving to the next set of sampling locations further down
             the length of each basin. In this way, corresponding areas in each basin
             were sampled and analyzed at about the same time during the sampling
             day.

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An efficiency factor (EF) based on the contact basin BODs loadings, air
volumes used, and mixed liquor dissolved oxygen concentrations was
calculated to investigate how the oxygen transfer efficiencies may have
changed during the periods between off-gas tests. Efficiency factors were
not calculated for the reaeration basins because the loadings were
unknown and could not be assumed equal because at times during the
study, each of the reaeration basins was used to supply return activated
sludge to two contact basins. The efficiency  factor calculations are
detailed in Appendix B and summarized as follows:

      EF             = BOD Loading / Qa / DO Correction
Where:

      BOD Loading   = BODs loading to the contact basin, Ib/day
      Qa             = air flow rate to the contact basin, cfm
      DO Correction  = dissolved oxygen correction factor
                      = (C*-C)/C*
      C*             = system saturation DO concentration, mg/1
      C              = contact basin mixed liquor
                         DO concentration, mg/1

While the efficiency factor is not an exact measure of the oxygen transfer
efficiency, it will provide a reasonable indication of how the oxygen
transfer efficiency changed, if the oxygen required per pound of BODs
remains constant, nitrification does not occur, and the dissolved oxygen
concentration used in the air flow rate correction is representative of the
weighted average concentration in the mixed liquor.

The constant oxygen requirement is not critical because the two test
quadrants are being compared and any changes in the oxygen.
requirement would be the same for both systems. Nitrogenous oxygen
demand was not observed during the study.

The DO correction factor is the greatest source of error. The value used
for C should be the air flow weighted average dissolved oxygen
concentration in the contact basin. The mixed liquor dissolved oxygen
concentrations used in the efficiency factor  calculations are computer
logged values based on measurements using one in-basin probe per tank.
While the single location near the outlet could provide dissolved oxygen
concentrations substantially different than the air flow weighted average,
the normal operating procedures used at the Green Bay plant minimized
the chances of error  because the dissolved oxygen uniformity was
checked several times a week and adjustments were made to the air flow
distribution if a substantial imbalance was found. Therefore, the average
of the single probe readings would normally be  indicative of the entire
tank contents.
                        10

-------
Diffuser Evaluations

Diffuser elements were tested at various times during the study to:
• Define the initial characteristics of the diffusers used in the study.

• Quantify changes in the diffuser characteristics caused by fouling or
   aging.
• Evaluate the effectiveness of preventive maintenance and restora-
   tive cleaning procedures.
All field monitoring was done  by GBMSD operations personnel.
Laboratory evaluations were performed by the Ewing Engineering
Company.

Both types of diffusers were characterized using dynamic wet pressure
(DWP) and steady state clean water oxygen transfer efficiency tests. The
ceramic diffusers were further evaluated using the bubble release
vacuum (BRV) test. Ceramic disc thickness and strength, and membrane
size, weight, hardness and modulus of elasticity were measured to
quantify any changes caused by aging.

DWP measurements were made in situ at the treatment plant and in a
laboratory at the Ewing Engineering Company. The  in situ
measurements were made  on the grid diffusers and  pilot diffusers.
Diffusers for laboratory testing were obtained from the removable pilot
headers or from the in-basin grids. Diffusers were collected from the
grids when the basins were drained for inspection and cleaning.

The steady state clean water oxygen transfer efficiency tests were run in
the laboratory in a 30-inch diameter by 10-foot water depth tank. Steady
state conditions were established  by feeding a constant rate of sodium
sulfite solution to maintain a dissolved oxygen concentration of 1.0 to 3.0
mg/1.  The oxygen transfer efficiency was measured using the  off-gas
method.

Although BRV tests can only be conducted on diffusers that are out of
service, the BRV test can be performed without removing the diffusers
from the basins. However, it was more convenient and more precise data
were collected by conducting the tests in the laboratory.

Indentation hardness of homogeneous materials ranging from soft
vulcanized rubbers  to some rigid plastics is  covered in ASTM
Specification D-2240. The specification covers type A (for softer
materials)  and type  D (for harder materials)  durometers and  the
procedure for determining the hardness. Indentation hardness was
measured using a type A dial  durometer. Five  locations on the
                        11

-------
membrane were measured and the results were averaged and reported
as Shore A Durometer hardness.

Modulus of elasticity is the ratio of the stress (stretching force per unit
area of cross-section) to the strain (elongation per unit length). It was
determined by measuring the diameter of the sheath at operating
pressures of approximately 5 and 15 inches of water gauge (w.g.). A
section of membrane between 2 and 2.5 diameters long was fixed on a
support with the ends sealed. An internal pressure tap was provided and
connected to a manometer to measure the static pressure within 0.5 in.
w.g. The diameter of  the membrane section was determined at  the
desired operating pressures by measuring the circumference of  the
cylindrical section using a pi tape, i.e., a flexible metal tape with 1- inch
markings at intervals equal to 3.1416 inches and each interval divided
into 0.005-inch graduations. The tensile modulus is calculated as follows:

       ET = (0.018) (Pis-PS) (Ds)2
                (Di5-D5)t

 Where:

       ET              = Tensile modulus of elasticity, psi
       P               = Pressure, either 5 or 15 in. w.g.
       D               = Membrane diameter at 5 or 15 in. w.g.,
                          inches
       t                = Membrane thickness, inches
Foulant Analysis

Foulant materials deposited on the diffusers were analyzed by the Ewing
Engineering Company as follows:

•  About 1 gram of the foulant (dry solids) was removed from a known
   area of the diffuser and analyzed for total solids.

•  The dried solids were crushed with a glass stirring rod and divided
   into two portions. One half of the dried solids were ignited at 600°C
   for 15 minutes to determine the volatile solids content.

•  The second portion of dried solids was mixed with about 10 ml of 14
   percent  HC1 in a Gooch crucible, steeped for about 10 minutes,
   washed with an additional 10 ml of 14 percent HC1 and rinsed with
   distilled water. The sample was then dried and the acid soluble frac-
   tion of the original sample was calculated.

•  The acid treated and dried solids were ignited at 600°C for 15 minutes
   to determine the volatile solids content of the acid insoluble solids.

Several samples of foulant were analyzed by electron dispersive
spectroscopy to determine the elemental constituents. The test measures
                        12

-------
            elements with atomic numbers greater than 10, i.e., carbon, nitrogen and
            oxygen are not measured.
RESULTS AND DISCUSSION
            The membrane tube diffuser system was installed first and put into
            service in January 1986. The ceramic disc diffuser system installation was
            completed in April 1986. To provide a clean start for both systems, the
            contact and reaeration basins equipped with the membranes were
            drained and the diffusers were cleaned by hosing, scrubbing with a stiff
            bristle brush, and rehosing. The cleaning procedure was recommended
            by the manufacturer. Both systems were then put  into service in May
            1986.

            The results of the various field and laboratory tests are presented and
            discussed in the following subsections:

             •  Operational procedures and goals
             •  Oxygen transfer efficiency versus time

             •  Oxygen transfer efficiency versus air flow rate

             «  Apparent alpha versus time
                                                                 i
             •  Pilot diffuser evaluations

             •  Grid diffuser evaluations

             •  Foulant analyses

             •  Cost analysis

            Operational Procedures and Goals

            In situ acid gas treatment of the ceramic diffusers and flexing of the
            membrane diffusers were  evaluated as preventive maintenance
            techniques for controlling diffuser fouling. For the first six months  of
            operation,  half of the ceramic grids were treated with HC1 gas  at
            frequencies ranging from monthly to every three months. Half of the
            membrane tube grids were flexed every three weeks. The frequencies
            were recommended by the equipment manufacturers. The preventive
            maintenance schedule is summarized in Table 4.

            The HC1 gas treatments were performed according to the manufacturer's
            instructions. Typically the acid gas is fed to the diffusers until the DWP
            is reduced to a predetermined value. Since there was little or no increase
            in DWP during the interval between treatments, it was decided to feed
            approximately 0.1 Ib HC1 per diffuser.
                                     13

-------
Table 4 - Diffuser Preventive
Quadrant 2 - Ceramic Disks
HC1 Gas Treatments
Frequency
Monthly
Monthly
Monthly
Every 2 Months
Every 2 Months
Every 2 Months
Every 3 Months
Every 3 Months
Grids
C2.1N
C2.2N
R2.1
C2.3N
C2.4N
R2.3
C2.5/6N
R2.5
Maintenance Summary
Quadrant 4 - Membrane Tubes
Flexing ;
Frequency
Every 3 Weeks
Every 3 Weeks
Every 3 Weeks
Every 3 Weeks
Every 3 Weeks
Every 3 Weeks
Every 3 Weeks
Every 3 Weeks
Grids
C4.1N
C4.2N
C4.3N
C4.4N
C4.5/6N
R4.1
R4.3
R4.5
The flexing procedure  was according to  the  membrane  diffuser
manufacturer's instructions. One grid was flexed at a time, by closing the
downcomer air valve, bleeding off the air in  the header system so the
membranes would collapse completely onto the frame, increasing the air
flow rate to  about  8 scfm per  diffuser for two to five minutes, and
returning the air flow rate to the previous operating level.

The operational goals throughout the study were to operate the two test
quadrants at  equal organic loadings, equal solids retention-times, and
equal dissolved  oxygen concentrations. Table 5  shows the  monthly
average data for these operating parameters from May 1986 through
October 1987.

Initially, 50 percent of the flow was fed to each of the two test quadrants
and the loadings were essentially equal. In mid-June  1986, it became
apparent that the two systems would not be able to handle the entire
load. The air usage was very high and it became difficult to maintain the
desired dissolved oxygen concentrations. At first, the problems appeared
to be worse in the ceramic system, so the plant staff decreased the BODs
loading  to that quadrant by putting one of the sparged turbine contact
basins in service. The resultant flow and loading split was 25 percent to
the ceramic system, 25 percent to the sparged turbine system, and 50
percent  to the membrane system. After about a week, adjustments were
made to equalize the loadings to all three contact basins. The third
contact basin remained in service through April 1987.

Reaeration basin 2 (ceramic system) supplied return sludge to contact
basin 2  (ceramic system)  and contact basin 1 (sparged turbines). The
hydraulics associated with this operating mode resulted in slightly higher
BODs loadings to the membrane system; however,  the differences
between the two test quadrants averaged about 5 percent.
                         14

-------
Table 5 -



Month
05/86
06/86
07/86
08/86
09/86
10/86
11/86
12/86
01/87
02/87
03/87
04/87
05/87
06/87
07/87
08/87
09/87
10/87
Average
Operating Data for May
Quadrant 2 -
BODs
Loading
1000 Ib/day
56.5
55.5
57.0
58.8
56.0
58.1
49.7
51.2
52.9
64.7
55.3
54.1
31.0
36.7
35.4
52.6
44.1
43.2
50.7
Ceramics

SRT
days
3.00
2.36
3.23
2.65
2.52
2.66
3.14
3.21
2.90
2.89
2.82
2.73
4.26
2.96
4.72
3.24
3.50
3.91
3.15

DO
mg/1
2.4
1.6
1.8
1.2
1.3
1.5
2.3
2.5
2.5
1.6
1.7
2.1
2.4
2.2
2.0
1.6
2.1
2.4
2.0
1986 - October 1987
Quadrant 4
BOD5
Loading
lOOlb/day
54.7
65.2
59.4
62.8
58.7
62.1
55.3
53.8
54.2
64.8
58.1
59.1
38.2
39.5
38.3
46.0
45.2
44.1
53.3
- Membranes

SRT
days
w«
3.02
2.36
3.03
2.86
2.86
2.87
3.37
3.64
3.42
3.26
3.09
2.92
3.67
2.74
4.91
3.55
3.98
4.11
3.31

DO
mg/1
~
2.3
1.6
1.8
1.4
1.6
1.6
1.8
2.5
2.4
2.1
2.0
2.0
2.2
2.0
1.8
1.8
2.0
2.3
2.0
Throughout the study, the solids retention times and dissolved oxygen
concentrations in the two quadrants were nearly equal.

Oxygen Transfer Efficiency Versus Time

Off-Gas Testing

The standard two-day off-gas test was conducted on the fine pore systems
nine times over the 18-month study period. The detailed data summary
tables are provided in a report by the Ewing Engineering Company.5 The
first six off-gas tests were conducted between the initial start-up in May
1986 and December 1986. The last three off-gas tests were conducted in
June, August and October 1987.

The in-process oxygen transfer efficiencies measured by  the off-gas
method were adjusted to standard conditions of 20°C, 1 atmosphere and
zero dissolved oxygen concentration. The adjusted in-process oxygen
transfer efficiencies are designated as alpha'-SOTE, where; the alpha'
                         15

-------
stands for apparent alpha. Alpha, defined as the ratio of the in-process
oxygen transfer coefficient to the clean water oxygen transfer coefficient,
is a function of the wastewater characteristics for a given system and
geometry. Apparent alpha includes other factors that affect performance
such as physical changes in the diffuser characteristics caused by fouling
and/or aging.

The results of the off-gas testing are shown in Figure 4. Each data point
is a basin average comprising the local data points weighted by the local
flux measurements as follows:

      Alpha'-SOTE = SUM [(Fi« alpha'-SOTEi)]/SUM [Fi]

Where:

      Alpha'-SOTE    = off-gas weighted basin average oxygen
                          transfer efficiency, decimal
      Fi               = local off-gas flux, scfm/sq ft
      alpha'-SOTEi    = local oxygen transfer efficiency, decimal
Each contact basin data point comprises 24 local measurements while
each reaeration basin data point comprises 12 measurements. The
December 1986 data points are an exception. The contact basin point
consists of 12 measurements and the reaeration basin point consists of
10 measurements. The December sampling plan was reduced because
daylight hours were limited.

The lines connecting the data points are provided to show the overall
changes in the alpha'-SOTE between test results. The lines are broken
in November 1986 and July 1987 to indicate that the systems were
drained for inspection and diffuser cleaning.

The significance of the differences in the off-gas weighted basin average
(mean) alpha'-SOTE values were evaluated using statistical tests. The
analysis of variance was used for the contact basin data while the t-test
was used  for the reaeration  basin data. The tests determine  the
probability that observed differences in the means are caused by random
rather than systematic variations. The analyses are based 'on a null
hypothesis that the means are equal. Then, if the test  indicates a high
probability that the difference is not caused by random variation, the
hypothesis is rejected and the conclusion is drawn that the  observed
difference in the means is significant. On the other hand, if  the
probability is low, it is concluded that the observed difference is  not
statistically significant A significance level of 0.05 was used  in all the
                         16

-------
  25



  20

UJ

015
CO
5io
     CONTACT BASIN
                          Cleaned
                          Diffusers
                                                Cleaned
                                                Diffusers
        56789  101112 1  23456789  1011
                 1986                     1987
25


20
LU

&
CO
   0
       REAERATION BASIN
^A   A	;	      \^
                                                    A—	^
        5  6  7  8  9  101112 1  2  3  4  5  6  7   8  9  1011

                 1986                     1987
       Legend
     o Ceramics
     A Membranes
                                  17
                                           FIGURE 4
                                           Oxygen Transfer Efficiency
                                           (Offgas Method) Versus Time

-------
tests. The significance level is the maximum probability of being wrong
if the null hypothesis is rejected.

Since the statistical tests only provide an insight into the relationship
between the sample mean and the sample variability, all the available
information should be considered before a final judgment is made. In
the case of analyzing the alpha'-SOTE data, additional information
regarding the oxygen transfer efficiency of the two test aeration systems
is available in the form of efficiency factors. These will be presented and
discussed in the next section. Details of the statistical analyses are
presented in Appendix C. The results are summarized in Table 6.

The contact basin alpha'-SOTE data depicted in Figure 4 show
discernible differences in all but two data sets, the July 30,1986 data and
the June 18, 1987 data. The statistical analysis of the data, however,
indicates that only the last two data sets are significantly different at the
0.05 significance level. The results of the statistical tests conducted on
the reaeration basin data confirm that the apparent differences shown in
Figure 4 are significant at the 0.05 confidence level.
Table 6 - Statistical Analysis of Alpha'-SOTE Data

Basin

Test Date
Contact 5-13-86








5-15-86
7-02-86
7-30-86
10-30-86
12-03-86
6-18-87
8-05-87
10-28-87
Reaeration 5-12-86








'No =
Yes =
5-16-86
7-01-86
7-29-86
10-29-86
12-02-86
6-17-87
8-04-87
10-27-87
Quadrant 2
Alpha'-SOTE
14.8
14.7
17.1
9.7
12.2
19.1
11.8
20.2
163
18.2
17.0
21.2
143
11.6
19.6
11.8
232
193
Quadrant 4
Alpha'-SOTE
163
162
17.0
12.1
143
163
11.4
12.1
113
17.6
17.0
18.4
112
13.4
13.1
11.1
13.7
12.7
Difference
Value
1.7
13
0.1
2.4
2.1
2.8
0.4
8.1
5.0
0.6
0.0
2.8
3.1
1.8
63
0.7
93
6.8
gig/
No
No
No
No
No
No
No
Yes
Yes
Yes
No
Yes
Yes
Yes
Yes
No
Yes
Yes
Differences are not significant at the 0.05 confidence level
Differences are significant at the 0.05 confidence leveL
                         18

-------
The lack of statistical significance in several of the contact basin
comparisons may be due to the inherent variability in the local
measurements caused by the high organic loadings, the high air flow rates
and the severe taper in the air flow rates between zones. The operating
data, presented in the next section in the form of efficiency factors,
support the conclusion that the discernible differences shown in Figure
4 are real.  In  the reaeration basins, the variability in the local
measurement of oxygen transfer efficiency was much smaller than in the
contact basins. The lesser variability was possibly due to lower organic
loadings resulting in more uniform air flow rates throughout the basins.

The two systems started out at nearly equal oxygen transfer efficiency.
The oxygen transfer efficiency of both systems  decreased substantially
such that after three months of operation, the oxygen transfer efficiency
was about 75 percent of the initial value. Rather than drain the basins
and clean the diffusers so early in the study, it was decided to continue
to operate with three contact basins in service and gain more operating
experience. In October 1986, the fifth off-gas test was conducted. The
off-gas test results indicated that the oxygen transfer efficiencies were
still substantially below the values measured in May 1986. There was also
a problem with maintaining acceptable DO concentrations at the inlet
end of the contact basins, so  it was decided to drain  the basins for
inspection and cleaning of the diffusers.

The cleaning methods employed were based on the results of evaluations
conducted in the laboratory on diffusers obtained from the removable
pilot headers. The  laboratory test results and proposed cleaning
procedures were discussed with and agreed to by  the manufacturers
before the cleaning activities were started. The first pilot diffusers tested
were ceramic discs from the reaeration basin. The foulant found on the
diffusers was in two layers. The top layer was slimy, about a 1/4-inch thick
and could be hosed off with water at a pressure of  about 30 psig. The
bottom layer was black, hard and firmly attached to the diffuser surface.
The black layer was soluble in 14 percent HC1 but the reaction was rather
slow. The cleaning procedure selected for use on the ceramic diffusers
was hosing from the tank top with fire hoses, partially filling the basin
with service water, gas cleaning with 0.1 Ib HC1 per diffuser, draining off
the service water, and rehosing from the tank top.

The foulant found on the contact basin diffusers was a single layer having
characteristics similar to the top layer found on the reaeration basin
ceramic diffusers. It was readily removed by hosing.  Tests on several of
the contact basin pilot diffusers indicated that the acid treatment step in
the cleaning procedure was probably not necessary because only a slight
improvement hi the clean water oxygen transfer efficiency was observed.
                         19

-------
However, it was decided to be conservative and perform the rigorous
hose, acid gas treat and rehose procedure anyway.

The membranes taken from the reaeration basin also had two foulant
layers. Membranes taken from the contact basin had a single layer. All
of the membranes were cleaned by hosing from the basin floor, scrubbing
with a stiff bristled brush, and rehosing. The procedure removed the
slime layer and the black material found on the reaeration basin units.
Tank top hosing was not attempted with the membrane tubes for two
reasons. First, there was concern that the force of the water falling from
a height of about 25 feet would break the connecting pipe nipples.
Second, the foulant was on both the top and the bottom of the diffusers
so tank top hosing would not have removed all of the foulant

Once the cleaning was complete, the systems were put back into service
and a followup off-gas test was conducted. The alpha'-SOTE of the
ceramic systems was essentially restored to its original condition in both
the contact and the reaeration basins, while the increases in alpha'-SOTE
in the membrane equipped basins were small.

The next off-gas test was conducted in June 1987. The measured oxygen
transfer efficiencies of the systems were similar to the oxygen transfer
efficiencies measured in October 1986 before the systems had been
cleaned. Based on the off-gas test results, the decision was made to drain,
inspect, and clean the two test quadrants. The  same cleaning methods
used in November 1986 were used in July  1987. The ceramic diffusers
were tank top hosed, acid gas treated, and rehosed. The membrane
diffusers were in-basin hosed, brushed, and rehosed. After cleaning, the
systems were put back into service and retested by the off-gas method.
The oxygen transfer efficiency of the ceramic system showed an increase
to above its  original level. The membranes showed little  if any
improvement.

The last off-gas test was conducted during the last week in October 1987.
The oxygen transfer efficiency of the contact basin ceramic diffuser
system decreased from nearly 25 percent to about 17 percent. A similar
reduction was experienced in the reaeration basin. The membrane
systems remained relatively constant at about 12 percent in the contact
basin and 13 percent in the reaeration basin.

Efficiency Factor

The efficiency factors for the two fine pore contact basins, calculated
from monthly average data, are plotted versus time in Figure 5. The
efficiency factor and the  off-gas results show similar trends. The
efficiency factors indicate that both systems lost oxygen transfer
                        20

-------
r
d  6
o
m
5  4
I
o>
'o
e
LU
  D
                    Cleaned
                    Diffusers
                      •'
Cleaned
Diffusers
5  6   7
                   8   9  10  11  12  1   2  345  6   78   910
                   1986                         1987
     Legend
   o Ceramics-
   A Membranes
     Based on the BOD5 loading and air flow rate to the contact
     basins and correcting the air flow rate to zero DO.
                                     FIGURE 5
                                     Contact Basin Efficiency
                                     Factor Versus Time
                                21

-------
efficiency after start up. The loss in efficiency was greater and more rapid
in the ceramic system, so over the first six months of operation, the
average oxygen transfer efficiency for the membrane system was higher.

After the November 1986 cleaning, the efficiency factor for the ceramic
system showed a substantial increase similar to the increase indicated by
the off-gas test results. The efficiency factor then decreased at a relatively
constant rate until the system was cleaned again in July 1987. During the
same time period, the efficiency factor for the membrane diffuser system
showed several monthly increases and then gradually decreased until the
system was cleaned in July. The rather large increase in the efficiency
factor seen in February 1987 is probably an outlier. The BODs loading
that month increased to both systems by 20 percent, but no additional
air was fed to the membrane quadrant. There may have been some
changes in the weighted average DO in the basin that were not accounted
for in the computer reported basin DO value.

The efficiency factor data from before and after the July cleaning show
that cleaning of the ceramic diffusers resulted in a substantial increase
in oxygen transfer efficiency. The membrane diffuser system showed
little or no increase in oxygen transfer efficiency after cleaning. The
ceramic diffuser system maintained a higher oxygen transfer efficiency
through to  the end of the study period in October 1987. These same
effects were indicated by the off-gas test results.

Oxygen Transfer Efficiency Versus Air Flow Rate

On three occasions, the air flow rates to the full-scale systems were varied
and off-gas tests were performed to investigate the relationship between
oxygen transfer efficiency and air flow rate per diffuser. The diffuser air
flow rates were adjusted by changing the total air flow rate to the basin
so any changes in the mixing pattern among grids would be minimized.
The number of hood positions sampled was reduced so several air flow
rates could be tested in one day.

The first test was performed on May 14,1986. One sampling position was
tested in each of the contact basins. The data are summarized in Table
7. The data show that the air flow rate per diffuser did not result in a
substantial change in alpha'-SOTE. However, because only one
sampling location was tested, the data are not conclusive. Changes in the
mixing among grids could have had a substantial effect on the results.

The  second and third tests were more extensive. Tests were conducted
before and after the July 1987 cleaning of the diffusers. Before the
cleaning effort, both the contact and reaeration basins were evaluated.
Five hood positions were sampled in each contact basin and four
                         22

-------
Table 7 - Variable Air
Flow Rate Testing - Mav 14. 1986
Contact Basin 2 - Ceramics1 Contact Basin 4 - M^mhran^c2
Air Flow
Rate, scfm
Total
13,600
13,600


17,000


7,000


13,600
7,000
1 Grid C2
2 Grid C4
/Unit
2.2
2.2


2.8


1.1


2.2
1.1
3NA
3NA
Time
hr
1210
1343
1353

1408
1418

1433
1444

1459
2151


Alpha' Air Flow Alpha'
-SOTE Rate, scfm Time -SOTE
% Total /Unit hr %
15.1 13,000 2.8 1517 15.2
15.2 17,000 3.7 1531 14.8
14.5
14.9 7,250 1.6 1544 12.3
16.9 13,000 2.8 1603 15.0
14.0
15.4 14,000 3.0 2135 14.3
14.9
15.2
15.1 ;
16.8 '
16.7 ' , ~


positions were used in the reaeration basins. After the cleaning effort,
the testing in the contact basins was repeated.

The alpha'-SOTE data are plotted versus sampling position in Figures 6
through 11. The results show that sampling position has a definite effect
on  alpha'-SOTE. Review of the data  collected from each Campling
position indicates that alpha'-SOTE is not affected substantially by
changes in the air flow rate per diffuser.

Apparent Alpha Versus Time

The basin average values of alpha' are  summarized in Table 8. Initial
values of alpha' for the contact and reaeration basins were in the range
of 0.46 to 0.53, substantially less than the design values of 0.68 and 0.90
for  the contact and reaeration basins, respectively. When fouled, the
range was reduced to 0.34 to 0.44. The lower alpha' values ;were the
reason why the two test quadrants could not treat the entire plant  load
and the third contact  basin had  to be operated. After the cleaning
activities in November 1986 and  July 1987, the ceramic system alpha'
                         23

-------
    25
    20
    15
 CO

 Q.
<
    10
                      OO
A
a
o
            C2.15
   Legend
   Basin Air Flow Rate
   6-23-87
   6,200 scfm
   12,200 scfm
   17,600 scfm
                      C2.2N
        C2.35
         Grid
C2.4N
C2.55
  Mean
Weighted
Average
   6-24-87
A  6,800 scfm
9  17,000 scfm
Diffuser Air Flow Rate

0.4 - 0.7 scfm/unit
1.3 - 1.7 scfm/unit
2.6 - 3.4 scfm/unit
                        0.9 - 1.2 scfm/unit
                        2.3 - 3.3 scfm/unit
                                    24
                         FIGURE 6;
                        Oxygen Transfer Efficiency;
                        Versus Position and Air
                        Fbw Rate  - Contact Basin
                        Ceramic Diffusers
                        Before Cleaning

-------
 LLJ
     30
     25
     20
 co
 jQ.
 <  ,
      0
              C2.IN
  Legend
  Basin Air Flow Rate
  8-6-87
a 10,500 scfm
o 17,100 scfm
C2.25
C2.3N
 Grid
C2.45
C2.5N
  Mean :
Weighted
 Average
 Diffuser Air Flow Rate


 0.9-2.6 scfm/unit
 1.5 - 3.1 scfm/unit
                                 25
                         FIGURE 7
                         Oxygen Transfer Efficiency;
                         Versus Position and Air
                         Flow Rate - Contact Basin •
                         Ceramic Diffusers
                         After Cleaning

-------
   18
   16
   14

llf

CO 12
 •
"co
.9-
< 10
                       O
            C4.IN
C4.25
C4.3N
 Grid
C4.45
C4.5N
   Legend
   Basin Air Flow Rate
   6-23-87
 A 7,400 scfm
 o 25,500 scfm

   6-24-87
 • 10,000 scfm
 • 21,400 scfm
  D iff user Air Flow Rate

  1.0 - 2.1 scfm/unit
  4.4 - 7.2 scfm/unit
 1.9 - 2.6 scfm/unit
 3.8 - 5.5 scfm/unit
  Mean
Weighted
 Average
                                26
                FIGURE 8
               Oxygen Transfer Efficiency
               Versus Position and Air
               Flow Rate - Contact Basin
               Membrane Diffusers
               Before Cleaning

-------
    18
    16
    14
I
CO  12
03

Q.
    10
    8
             C4.IN
C4.25
C4.3N
 Grid
C4.45
     Legend
     Basin Air Flow Rate
     8-6-87
  A  9,900 scfm
  o  18,200 scfm
     Diffuser Air Flow Rate


    2.0 - 2.4 scfm/unit
    3.7 - 4.3 scfm/unit
                                          Cfc
C4.5N
  Mean
Weighted
 Average
                                  27
                            FIGURE 9
                            Oxygen Transfer Efficiency
                            Versus Position and Air
                            Flow Rate - Contact Basin
                            Membrane Diffusers
                            After Cleaning

-------
18

16
o 14
uF
Q
CO 12
1
"co
Q.
<10
8
6
• n & 0.5
°1.3
O2.5
• " :
•

D2.2
02.9 24
DD^i.o
2.0
1
D 2.0
O1.4
131.85
A1X> CP2.7
D2.0 2.5 A 1.7
•
• • • • f| § • R ••
R2.1 R2.3 R2.4 R2.6 Mean
Grid Weighted
Average
Legend
Basin Air Flow Rate
A * 2,250 scfm
a * 4,200 scfm
     5,100 scfm
  * Air Flow Rate/Diffuser
                                    28
 FIGURE 10
Oxygen Transfer Efficiency
Versus Position and Air
Flow Rate - Reaeration Basin
Ceramic Diffusers
Before Cleaning

-------
          18
          16
          14
o
CO
 I
"ctt
 cL
          12
          10
          8
                                D3.0
                               1.6
                                  Q4.7
                                   £1.7
                                    Q2.7
                                                1.6
              n 3.0
             £1.9

            3.9   O 4.5
                             4.7
                                  4.6
                                                   Q4.8
            A1.7

          4.5 Da.o
                                                     Q3.4
                 R4.1
                      R4.3       R4.4
                           Grid
R4.6
      Legend
      Basin Air Flow Rate
A  *  2,350 scfm
n  *  4,240 scfm
o  *  6,300 scfm
   *  Air Flow Rate/Diffuser
  Mean
Weighted
. Average
                                       29
                                         FIGURE 11
                                         Oxygen Transfer Efficiency
                                         Versus Position and Air
                                         Flow Rate - Reaeration Basin
                                         Membrane Diffusers
                                         Before Cleaning

-------
Table 8 - Apparent Alpha as a Function of Time in Service
Time in Service, months
Basin
Contact
Reaeration
Contact
Reaeration
Contact
Reaeration
Contact
Reaeration
Contact
Reaeration
Contact
Reaeration
Contact
Reaeration
Contact
Reaeration
Total Since Cleaning Apparent Alpha
Ceram Memb Ceram Memh Ceram Memh
<1
2
2
3
3
6
6
7
7
13
13
15
15
18
18
4
4
6
6
7
7
10
10
11
11
17
17
19
19
22
22
<1
2
2
3
3
6
6

-------
Table 9 - Diffuser Characterization
New Ceramic Discs
Diffuser No.
K-39-40-1
K-39-40-2
K-39-40-3
K-39-40-4
K-39-40-5
K-39-40-6
K-39-40-7
K-39-40-8
K-39-40-9
K-39-40-10
K-39-40-11
K-39-40-12
K-39-40-13
K-39-40-14
K-39-40-15
Average

0.5cfm
4.90
4.90
5.05
4.70
4.80
4.70
5.00
4.90
5.00
5.00
5.00
4.95
4.80
4.85
4.95
4.90
Coefficient of variation,
DWP,
0.75 cfm
5.20
5.20
5.35
5.00
5.10
5.05
5.35
5.25
5.25
5.35
5.30
5.25
5.10
5.10
5.20
5.20
in. w.g.
2.0 cfm
5.90
5.75
6.00
5.60
5.70
5.50
6.00
5.70
5.95
5.85
5.80
5.90
5.60
5.60
5.95
5.79
Results -

3.1 cfm
7,05
6.75
7.30
6.70
6.85
6.35
7.40
6.60
7.20
7.00
6.80
7.15
6.55
6.45
7.15
6.89
BRV^
Mean
5.98
6.06
6.09
5.59
5.67
5.67
6.03
6.03
6.09
6.01
6.24
6.03
5.80
5.71
5.78
5.91
in. w.g.
COV1
0.032
0.032
0.021
0.032
0.026
0.025
0.020
0.035
0.029
0.019
0.031
0.022
0.030
0.040
0.032
0.033
standard deviation/mean. :
Table 10 - Diffuser Characterization Results -
New Membrane Tubes

Diffuser No.
K-38-43-1
K-38-43-2
K-38-43-3
K-38-43-4
K-38-43-5
K-38-43-6
K-38-43-7
K-38-43-8
K-38-43-9
K-38-43-10
K-38-43-11
K-38-43-12
K-38-43-13
Average

l.Ocfm
6.15
7.50
7.10
7.80
7.20
7.30
7.20
7.00
7.60
7.60
7.50
7.00
7.30
7.25
DWP,
3.0 cfm
8.90 .
9.80
9.80
9.70
9.90
9.90
9.65
9.30
10.0
9.60
9.90
9.80
9.00
9.70
Shore A Durometer, average of five
in. w.g.
6.0 cfm
10.7
11.2
12.5
11.8
12.3
12.6
12.0
11.7
12.5
11.8
12.5
12.5
12.4
12.0
points.
!
Hardness1 Weight
9.0 cfm
13.5
13.8
14.2
13.2
13.7
14.5
13.5
13.2
14.1
13.2
14.2
14.3
14.0
13.8

Mean
64.8
_
64.0
60.5
64.0
_
60.4
63.7
65.2
61.8
_
63.1
64.4
63.2

Grams
_
118.7
_
_
_
118.7
—
—
_
.
^
_
118.9
118.8
i
31

-------
Table 11 - Ceramic Diffuser Test Results -
Pilot Units Removed June 11, 1986
DWP,in.w.g.
Diffuser
No.
K-39-40-3
K-39-40-3
K-39-40-6
K-39-40-6
K-39-40-7
K-39-40-7
K-39-40-8
K-39-40-8
K-39-40-11
K-39-40-11
Condi
tion
New
Used2
New
Used2
New
Used3
New
Used3
New
Used4
0.5
cfm
5.05
8.30
4.70
8.80
5.00
6.50
4.90
7.00
5.00
6.25
0.75
cfm
535
9.40
5.05
10.2
5.35
7.55
5.25
7.65
530
7.10
2.0
cfm
6.00
14.8
5.50
17.6
6.00
11.7
5.70
12.5
5.80
10.7
K-39-40-12 New 4.95 5.25 5.90
K-39-40-12 Used4 5.85 6.65 9.60
1 Coefficient of variation, standard deviation/mean.
2 From pilot header R2.2P.
3 From pilot header C2.6SP.
4 From pilot header C2.2SP.
3.1
cfm
7.30
25.6
635
33.8
7.40
22.1
6.60
23.5
6.80
20.9
7.15
16.8
BRV.iiLw.fi.
Mean
6.09
27.2
5.67
25.9
6.03
19.0
6.03
19.0
6.24
18.5
6.03
16.0
cov1
0.021
0.179
0.025
0.191
0.020
0.211
0.035
0.164
0.031
0.303
0.022
0334
flow rate to the pilot header was reduced to account for the decreased
number of diffusers.

Summer 1986

On June 11, 1986, the Sanitaire pilot headers were removed to install
new air control orifices. While the headers were out, several; discs from
the contact and reaeration basins were tested on-site. The results of the
tests are summarized in Table 11. A substantial quantity of foulant
material was found on the surface of the discs. The material appeared to
be a slime growth containing a gritty sand-like material. The BRV and
DWP data indicate that the diffusers were moderately fouled.

During this site visit, the plant staff reported that the flow rate of air to
maintain acceptable DO concentrations was 10 to 15 percent higher for
the contact  basin 2 ceramic discs compared to the contact basin 4
membrane tubes. To evaluate the situation, several more pilot diffusers
were removed and tested in the laboratory. Two diffusers were tested as
received. One was then HC1 gas cleaned, retested, hosed off with a 40
psig water spray at about 20 feet, and tested again. The results of the tests
are summarized in Table 12.
                         32

-------
             The units, which had been in service in the contact basin for about 105
             days, showed a decrease of about 7 percent in clean water oxygen transfer
             efficiency. A single cycle  of acid gas cleaning produced no immediate
             improvement in oxygen transfer efficiency but a decrease in DWP did
             occur. Light hosing restored the clean water oxygen transfer efficiency
             to approximately its new condition. Further acid treatment and hosing
             produced no further improvement in oxygen transfer efficiency. Light
             hosing of a fouled disc which had no prior acid treatment restored it to
             near its estimated  original condition.

             For comparison, a  membrane tube diffuser was also removed and tested.
             The DWP of the  diffuser was only slightly higher than the measured
             average for the new diffusers. The clean water oxygen transfer efficiency
             of the used diffuser which was in service for about 87 days was essentially
             equal to a new diffuser.

             The observed need for more air in the contact basin with the ceramic
             diffusers was further investigated  by removing another pilot diffuser in
             August 1986. The diffuser was clean water tested at air flow rates of 1.0,
             2.0 and 2.8 cfm to determine if the relationship between oxygen transfer
             efficiency and air flow rate was different for a fouled diffuser than for a
             clean  diffuser. A change in the relationship was seen at Lansing,
             Michigan. The test results showed that the relationship was essentially
             the same for both a clean and the fouled  diffuser. In both cases,  the
 Table 12 - Ceramic Diffuser Test Results -
	Pilot Units Removed June 22,1986
DWP, in WG

Condition
Newz
^
As Found
/\
HC1 Gassed2
Hosed2'3
H-A-H2'4
0.5
cfm
4.80
7.85
_
4.80
0.75
cfm
5.10
11.8
_
6.20
5.20
2.0
cfm
5.60
-
—
7.85
6.10
3.1
cfm
6.55
.
_
11.3
8.00
BRV, in w.g.

Mean
5.80
_

8.61
5.68

COV
0.030


0.097
0.015
CWOTE
Ratio to
Control1
_
0.89
084
U.OH
0.98
i.m
New0
Hosed3'5
4.85
6.00
5.10
6.50
5.60
8.00
 6.45
11.3
5.71
7.06
0.040
0.075
                                                                       1.04
  Clean water oxygen transfer efficiency at 1 cfm measured by the small-tank steady state method and
compared to diffuser "C" used as the control.
3 Diffuser number K-39-40-13 mounted on pilot header number C2.1NP.
  Hosing done with 40 psig water from a distance of 20 feet.
  Hose-acid-hose, 14% HC1 sprayed on the diffuser and left for 20-30 seconds before rehosing.
  Diffuser number K-39-40-14 mounted on pilot number header C2.1NP.
                                     33

-------
oxygen transfer efficiency was proportional to the air flow fate to the
-0.21 power.

October 1986

Three ceramic disc diffusers and three membrane tube diffusers were
removed from the pilot headers in October 1986 for routine testing. The
discs were removed on October 21 and the membranes were removed
on October 28.

The ceramic disc diffuser taken from the inlet end of the contact basin
(C2.2SP) was tested ias found, after an acid gas treatment in the
laboratory and after hosing with a 30 psig water stream for 30 seconds.
The results of the tests are summarized in Table 13. The diffuser in the
as-found condition was fouled with a slime layer. The DWP and BRV
data indicate that the diffuser was moderately fouled. The clean water
transfer efficiency was reduced by about 25 percent A single acid gas
treatment did not improve the clean water transfer efficiency. The light
hosing, however, resulted in a substantial increase in clean water transfer
efficiency. Similar tests were conducted on a diffuser from pilot header
C2.6NP located near the outlet end of the contact basin. The test results
again showed low pressure hosing was effective in restoring the clean
water transfer efficiency.

The ceramic diffuser taken  from the inlet end of the reaeration basin
(R2.2P) was more fouled than the contact basin diffusers. DWP and
BRV measurements were slightly higher while the clean water oxygen
transfer efficiency was slightly lower. Hosing effectively removed the
loosely attached slime layer, but a black splotchy material remained on
the surface of the diffuser after hosing. Despite the black material, the
clean water oxygen transfer efficiency improved by about 28 percent.
Because the black material was not readily dissolved by treating with 14
percent HC1, an attempt was made to remove the material by wire
brushing. The clean water oxygen transfer efficiency of the wire brushed
diffuser was higher than the diffuser just after hosing but the DWP and
BRV remained moderately higher than a new diffuser.

The membrane diffusers were collected from the inlet (C4.2NP) and
outlet (C4.6SP) ends of the contact basin and from the inlet end of the
reaeration basin  (R4.2P). The clean water oxygen transfer  efficiency
tests were conducted  in parallel with a new  membrane diffuser
designated GBN. The results of the tests are summarized in Table 14.

The diffusers were covered with a slime material  similar to that found
on the ceramic discs. The slime material was easily removed by low
pressure (30 psig) hosing, brushing, and rehosing. The diffuser from the
                        34

-------
Table 13 - Ceramic Diffuser Test Results -
Pilot Units Removed October 21, 1986

DWP
Diffuser @ 2 cfm
No. Condition in. w.g.
K-39-40-11^ New 5.80
As Found 21.8
After LGC

After H/30 9.0
K-42-3-13 As Found 21.2
After Stor
After H/60 10.5
K-39-40-34 New 6.00
As Found 29.1

After Hose
After WB/H 8.80
Typical New (Table 9) 5.79
A new diffuser designated C was used as the control
2 From pilot header C2.2SP.
3 From pilot header C2.6NP.
4 From pilot header R23P.
Key: LGC = Laboratory gas cleaned
BRV,


Mean
6.24
28.9
-

12.9
24.7
-
143
6.09
32.0

-
10.2
5.91





in. w.g.


COV
0.031
0.200
-

0.230
0.140
-
0.130
0.021
0360

-
0.15
0.033





CWOTE
Ratio to
Control1
@cfm
_
0.77 @ 1.0 ,
0.79 @ 1.0
0.70 @ 2.0
0.91 @ 2.0
0.81 @ 1.0
0.89 @ 1.0
1.07 @ 2.0
«•
0.86 @ 1.0
0.68 @ 2.0
0.88 @ 2.0
0.99 @ 2.0
-





H/30 = Low pressure (30 psig) hosed for 30 seconds
H/60 = Low pressure hosed for 60 seconds



WB/H = Wire brushed then low pressure hosed
reaeration tank had a black crusty layer under the slime layer which also
was removed by the hose-brush-hose procedure. The DWP of the dirty
diffusers was slightly higher than GBN and several inches higher than
the average of 13 new diffusers tested at the beginning of the study. After
cleaning, the DWP of the pilot diffusers was substantially less than the
DWP of new diffusers. The clean water oxygen transfer efficiency of the
fouled  diffusers was significantly less than GBN. Clean waiter oxygen
transfer efficiency tests were not conducted at  this time on the
hosed-brushed-hosed diffusers so no comparison between dirty and
cleaned diffusers could be made.

November 1987

At the  end of the study, several ceramic and membrane diffusers were
taken from pilot headers and tested to determine the characteristics of
                        35

-------
Table 14 - Membrane Diffuser Test Results - Pilot Units
Removed October 28, 1986

Diffuser From
No. Header Condition
K-42-16-1 C4.2NP As Found
After H-B-H
K-42-16-2 C4.6SP As Found

K-42-16-3 R4.2P As Found
After H-B-H
Typical New (From Table 10)
GBN

DWP@
2cfm
in. w.g.
11.2
6.60
11.9

14.9
4.00
8.60
11.2
A new diffuser designated GBN was used as the control
Key. H-B-H = Low pressure (30 psig) hosed, brushed with
and rehosed.
CWOTE
Ratio to
Controll
<5>cfm
0.74 @ 1.0
0.85 @ 1.0
0.85 @ 2.8
0.71 @ 1.0
0.74 @ 2.8
-
1.0
a scrub brush
diffusers that had been in service for the entire 18-month period. The
diffuser test results provided some unique information because none of
the units had ever been cleaned.

The results of the tests conducted on three ceramic diffusers taken from
contact basin pilot header C2.6SP and three diffusers taken from
reaeration basin R2.6P are presented in Table 15. All the diffusers were
very fouled, based on DWP, BRV, and clean water transfer efficiency
measurements. Treating with HC1 gas substantially reduced the DWP,
but not to like-new condition. Several of the diffusers were cleaned using
a more rigorous three-step procedure. The units were hosed, sprayed
with a 14 percent solution of HC1, allowed to stand for 15 to 20 minutes,
and hosed again (H-A-H). This treatment further reduced  DWP. The
BRVs of the H-A-H cleaned diffusers were substantially reduced but
remained moderately higher than typical new units, and the coefficient
of variation (COV) of BRV increased indicating a loss in uniformity.

The fouled ceramic diffusers had clean water oxygen transfer efficiencies
that were 17 to 34 percent lower than a typical new diffuser. After
                         36

-------





















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-------
cleaning by the H-A-H method, the clean water oxygen transfer
efficiency was restored to about 95 percent of a typical new diffuser.

Diffusers K-49-40-8 and K-49-31-2 were fractured and photographs of
the cross-section were taken at a magnification of 15X (Figure 12).
Entrapped residues were limited to near the surface. The penetration
was approximately 500 microns (0.02 in.).

The exponent of the clean water oxygen transfer efficiency versus
diffuser air flow rate relationship was negative for both the new and used
diffusers, i.e., the oxygen transfer efficiency decreased when the diffuser
air flow rate was increased. The absolute value of the exponent for the
used diffusers, either fouled or cleaned, was greater than for the typical
new ceramic diffuser. For a new diffuser, increasing the air flow rate/unit
from 1.0 cfm to 3.0 cfm would result in a 15 percent decrease in the clean
water oxygen transfer efficiency. Using an average value of-0.21 for the
exponent of the used diffusers, increasing the diffuser air flow rate from
1.0 cfm to  3.0 cfm results in a 21 percent decrease in the clean water
oxygen transfer efficiency. This shows the importance of operating the
diffusers at the lower end of their normal design range.

The results of the tests conducted on three membrane diffusers taken
from contact basin pilot header C4.6NP and three diffusers taken from
reaeration basin R4.6P are presented in Table 16. All of the membranes
were moderately fouled based on the DWP data. At 1.0 cfm, the DWPs
were not noticeably higher than a typical new membrane. At 3.0 cfm, the
DWPs were substantially higher than a typical new diffuser. Cleaning by
hosing, brushing with a stiff bristle scrub brush, and rehosing (H-B-H),
or by inside-out flushing of the slits with a 3 to 5 gpm of clean water while
brushing the entire outer surface with a stiff nylon brush (FB) resulted
in DWPs that were substantially lower than the typical new membrane.

Air flow uniformity was determined by measuring the discharge rate
from five  sections  along  the length of the membrane while it was
operated  at 2 scfin. The  results are presented as the coefficient of
variation (COV) equal to the standard deviation divided by the mean.
The typical value of COV is 0.24. Even the most fouled diffusers had
relatively good uniformity, the highest value being 0.52. Cleaning the
units improved air flow uniformity with values of COV ranging from 032
to 037.

The clean water oxygen transfer efficiencies of the fouled membranes
were about 35 percent less than typical new membranes at 1.0 cfm, and
about 25 percent less at 3.0 cfm. The greater loss in clean water oxygen
transfer efficiency at the lower diffuser air rate is also indicated by the
change in exponents for the oxygen transfer efficiency versus diffuser air
                         38

-------
                                                   Contact Basin

                                                   Macrograph
                                                   C40687 (15x)
Cross-Sections Show Entrapped Residues to
a Depth of About 500 Microns (0.02 inches)
                                                  Reaeration Basin

                                                  Macrograph
                                                  C40688 (15x)
                                   39
                                           FIGURE 12
                                           Photographs of Fractured
                                           Ceramic Diffusers

-------



















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flow rate relationship. The exponent determined for the new diffusers
was negative which is typical for fine pore diffusers while the used
membranes (both as found and cleaned) showed positive exponents. The
exponent data indicate that there may be some advantage to operating
at slightly higher air flow rates, or, conversely, that operating at higher
diffuser air flow rates over the range tested would not result in losses in
oxygen transfer efficiency as would be expected from the new diffuser
test data.

Dimensional and weight changes over the 18-month period were small.
The tensile modulus, which is  a measure of a material's stiffness
increased substantially, indicating that the material physical properties
had changed. Photographs of these units were not taken because several
grid units had already been photographed. The membrane photographs
are presented in the next section.

Grid Diffuser Evaluations

Diffusers were removed for testing when the basins were drained in
November 1986 and July 1987.

November 1986

The results of laboratory tests conducted on  the  ceramic diffusers
removed before and after the November 1986 cleaning are presented in
Figure 13. As previously described, the grid units were cleaned by hosing,
treating with HC1 gas and rehosing, labeled H-AG-H in Figure 13. The
units designated as being acid gassed were given the treatment in situ on
the frequency listed in Table 4.

The fouled diffusers from the contact basin showed moderate increases
in BRV and DWP, and substantial  reductions  in clean water oxygen
transfer efficiency. The diffusers taken from the inlet end had higher
BRVs, DWPs and lower clean water oxygen transfer efficiencies than the
diffusers taken from the outlet end. Because the foulant consisted of a
loosely attached slime-like layer, it was effectively removed by a water
spray directed from the basin walkways using fire hoses. Acid gas
treatment and rehosing provided little if any further improvement in
BRV, DWP or clean water oxygen transfer efficiency. Regular acid gas
treatment may have provided some control of DWP increase but did not
prevent losses in oxygen transfer efficiency.

Visual observations made after draining the reaeration basin indicated
that the diffuser fouling was two-layered, a slime-like layer similar to that
found in the contact basin over a hard black layer. The fouling was
relatively uniform from the inlet to the outlet end. Tank top hosing
                         41

-------
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                                 42
 FIGURE 13
Ceramic Diffuser Test Results -
Grid Units Removed November 1986

-------
removed the slime- like layer but not the black splotchy layer. The black
material contained substantial amounts of iron and it was slowly soluble
in 14 percent HC1. Treating with HC1 gas and rehosing from the tank top
improved the diffuser characteristics but most of the black layer
remained. The diffusers  that received the monthly in situ acid gas
treatments appeared to have the least amount of the black foulant on the
surface of the discs.

The results of the tests conducted on the membrane diffusers removed
before and after the November 1986 cleaning are presented in Figure
14. The cleaning procedure was the previously described hose, brush and
rehose (H-B-H) method. The flexing of selected grids was done every
three weeks.                                          ;

The diffusers in the contact basin were more fouled at the outlet than at
the inlet end. Many of the diffusers in the first aeration zone looked clean
while the diffusers in the second and third zones were covered with about
a quarter-inch of a slime-like material.  Large quantities of grit had
accumulated at the inlet end especially where the diffusers were the
cleanest. The grit may have provided some cleaning by abrasion. The
high liquid velocity in this area of the basin (between zones 1 and 2) was
the result of the significant differences in air rates used in the two zones.
The air flow rates to zone 1 were typically more than 50 percent higher
than in zone 2.

Cleaning improved the clean water oxygen transfer efficiency of the
membranes taken from the outlet end but not the one collected from the
inlet end. Cleaning did not restore the clean water oxygen transfer
efficiency to a like-new condition. The inability to restore the clean water
oxygen transfer efficiency may have been caused by changes in the
membrane materials as indicated by the lower than new DWPs of the
cleaned diffusers.

The observations made and the data collected on diffusers from the
reaeration basin before and after cleaning indicate that the fouling was
relatively uniform from inlet to outlet. The foulant was similar to that
found on the ceramic diffusers. It consisted of two layers, a slimy material
over a hard black crusty material. Both layers were effectively removed
by in-basin hosing, brushing and rehosing as evidenced by the after
cleaning DWPs and visual observations.

The DWPs  of the dirty diffusers were not much different than the
average new membrane. Cleaning of the membranes lowered the DWP
substantially below the typical value for a new membrane and the clean
water oxygen transfer efficiency after cleaning did not approach the level
attained by a new diffuser such as GBN.

-------
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                             Grid & Condition
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FIGURE 14
Membrane Diffuser Test Results -
Grid Units Removed November 1986
                                44

-------
Flexing of the membrane diffusers did not control the fouling in either
the contact or the reaeration basin. DWPs measured on the flexed and
unflexed diffusers were nearly equal. This is consistent with observations
that the air flow rate to a recently flexed grid, if left unthrottled, was
greater than the air flow  rate to the unflexed grids because the
relationship between DWP and air flow rate is such that small differences
in DWP result in large differences in air flow rate. The clean water
oxygen transfer efficiency  of the fouled diffusers both flexed  and
unflexed were nearly equal.

Because the benefits of the in situ acid gas treatments of the ceramics in
the contact basin were minimal, the number of grids receiving the
preventive maintenance treatment was reduced. Starting in December
1986, only one grid (C2.2N) in contact basin 2 was given monthly in situ
acid gas treatments.  On the other hand, five of the six grids in the
reaeration basin (R2.1 through R2.5) were acid gas treated monthly
because the acid treatments appeared to minimize the black foulant layer
which was encountered in this basin.

The number of membrane tube equipped grids that were flexed was also
reduced from half to  two in  the contact basin (C4.2N and C4.4N), and
one in the reaeration basin (R4.1).

July 1987

The results of the laboratory tests conducted on the ceramic diffusers
removed in July 1987 are presented in Figure 15. The diffusers taken
from the contact basin showed moderate increases in BRV and DWP
except for  the  diffuser  that did not receive the  monthly acid gas
treatments. The BRV measured for.the untreated diffuser was 23.6
inches of water gauge (w.g.). The unit that received monthly acid gas
treatments  showed a smaller increase  in BRV and DWP than the
untreated unit.  The rigorous hose, acid gas and rehose cleaning
procedure restored the BRV and DWP of both units to a like-new
condition.

The units taken from the reaeration basin had higher BRVs and DWPs
than the units taken from the contact basin. The unit that received
monthly acid treatments was less fouled, having a lower BRV, DWP and
visibly less of the black deposits. The DWPs of both units were returned
to a like-new condition after cleaning by the hose, acid gas, and rehose
method. However, not all of the black foulant material was removed by
the cleaning effort

The fouled ceramic diffusers from the contact and reaeration basins
showed losses in clean water oxygen transfer efficiency  of about 25
                        45

-------
    CONTACT BASIN
REAERATION BASIN
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     46
FIGURE 15
Ceramic Drffuser Test Results -
Grid Units Removed July 1987

-------
percent. In the contact basin, the acid gas treated diffuser had a higher
clean water oxygen transfer efficiency than the untreated unit. However,
the number of diffusers tested was small so it is not possible to determine
if the monthly  acid gas treatments provided a real benefit in terms of
limiting losses in clean water oxygen transfer efficiency. For the contact
basin units, the hose, acid gas, and rehose cleaning procedure resulted
in an increase in the clean water oxygen transfer efficiency to about 95
percent of new.

The clean water oxygen transfer efficiency of the all diffusers taken from
the reaeration basin were essentially equal. The increase in clean water
oxygen transfer efficiency after cleaning was less for the diffusers from
the reaeration basin.

The results of the July 1987 laboratory tests conducted on the membrane
diffusers are presented in Figure 16. The DWPs of the fouled diffusers
taken from the contact basin were less than or equal to a typical new
diffuser. Fouled diffusers from the reaeration basin showed moderate
increases in DWP. Cleaning by the hose, brush,  and rehose method
reduced the DWP of all the units to a level substantially less than a new
diffuser. The clean water oxygen transfer efficiency of the fouled and
cleaned diffusers were essentially equal. Flexing of the membranes did
not appear to provide any benefit over not flexing.

Several of the used membrane diffusers were further evaluated  to
determine which membrane characteristics, if any, had changed. The
membranes were measured, weighed and  tested  for elasticity and
hardness. The results of the measurements and tests are summarized in
Table 17. All of the membranes tested showed changes in dimensions,
weight and elasticity. Hardness was essentially unchanged.

The average increase in diameter was about 0.11-inch or 5 percent while
the average membrane thickness was reduced by about 0.0025-inch or 8
percent. The membrane material  became stiffer  as indicated by the
relatively large increase in tensile modulus. These quantitative changes
are in addition to the visual observations made during the diffuser testing
which indicated that the slits in the used membranes were wider than the
ones in the new membranes and that the slits did not close completely
after the air was shut off. The changes in the slits were documented by
photographing new and used membranes operating at 10 in. w.g. The
used membranes were cleaned either by the hose, brush and rehose
method or by flushing the slits with clean water from the inside out while
brushing. The flushing method was suggested by the membrane diffuser
manufacturer. Several of the photographs, taken by Midwest Research
Microscopy Inc. (Milwaukee, WI), are reproduced in Figures 17,18 and
                        47

-------
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FIGURE 16
Membrane Diffuser Test Results
Grid Units Removed July 1987!
                                48

-------
             3
 n
« r
.  ! t  <  11
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-------
       New Membrane Operating at DWP of 10 in. w.g.
Used Contact Basin Membrane Operating at DWP of 10 in. w.g.
                                    FIGURE 18
                                    Photographic Comparison
                                    New Versus Flush/Brush
                                    Cleaned Contact Basin
                                    Membrane Diffuser
                           50

-------
        New Membrane Operating at DWP of 10 in. w.g.
Used Reaeration Basin Membrane Operating at DWP of 10 in. w.g.
                            51
FIGURE 19
Photographic Comparison -
New Versus Hose-Brush-Hose
Cleaned Reaeration Basin
Membrane Diffuser

-------
Table 17 • Comparison of New and Used
Grid/Flexed Weight Length Diameter
DiffuserNo. gm. in. in.
Typical New
Mean 120
Sample Size 8
COV2 0.02
"R4.4/No~ 	 ""
K-45-65-1 112
R4.5/Yes
K-45-65-3 114
C4.4N/Yes
K-45-67-2 114
C4.4S/NO
K-45-67-3 113
G4.2N/Yes
K-45-67-5 111
C4.2S/NO
K-45-67-6 118
Average 114
263
5
0.01
25.0
25.1
25.7
25.4
25.7
26.0
25.5
2.25
5
0.01
236
237
233
239
239
233
236
Membranes
;
Thick- Tensile
ness Modulus Hard
in. psi ness1
0.0311 630
8
0.05
0.0280
0.0278 940
0.0280
0.0272 860
0.0263
0.0287
0.0277 900
Percent
Change3 -42 -2.7 +4.9 -83 +45
1 Shore A Durometer, average of five points on the membrane, from Table 10.
2 Coefficient of variation, standard deviation/mean.
3 100 x (Used - New)/(New)
63.2
10
0.03
63.1
62.5
61.4
63.1
635
62.7
633
-0-5
19. The slits in all the used membranes were wider than the slits in a
typical new membrane.

Foulant Analysis

Samples of foulant materials were collected from several ceramic disc
and membrane tube diffusers after they were removed from; the contact
and reaeration basins during November 1986 and July 1987.

The diffusers  taken from the reaeration basins were covered by two
foulant layers. The outer layer was a loosely attached slime-like material
that could be removed by hosing with water at a nozzle discharge
pressure of 30 psig. Visual and tactile observations indicated that this
layer comprised biological slime into which a gritty, sand-like material
was incorporated. A photograph of a cross-section of the slime layer is
presented in Figure 20.
                         52

-------
Metallographically Polished Cross-Section of
Residues Showing a Variety of Particles
Similar to Soil or Rock.
                                                     Contact Basin

                                                     Macrograph      !
                                                     C40689 (100x)
                                              FIGURE 20
                                              Photograph of Foulant
                                              From a Contact Basin
                                              Ceramic Diffuser
                                 53

-------
The inner layer was black, hard, and firmly attached to the surface of the
diffusers. Analysis of  the  black foulant by electron dispersive
spectroscopy showed that the  major constituents were iron (18.5
percent) and calcium (32 percent). On the ceramic diffusers, this layer
was not uniformly distributed. When the outer layer was removed, the
inner layer looked like splotches of black tar. The distribution of this
foulant on the membrane diffusers was not readily discernible because
the membrane material was also black.

The results of analyses conducted on the foulant samples taken from the
ceramic diffusers are summarized in Table 18. The  mass of the slimy
foulant layer varied substantially from diffuser to  diffuser, and the
variations were random, i.e., there was no clear pattern of more foulant
at a basin inlet or outlet end. The regular acid gas treatments did not
substantially reduce the slimy foulant mass deposited on a diffuser even
though it resulted in a marked reduction in DWP. The volatile fraction
of the slimy layer was relatively constant with values between 13 and 24
percent. The low volatile content is explained by the presence of the
gritty material which was probably sand particles.  The acid gas
treatments did reduce the acid soluble fraction in the foulant layer but
this was not a substantial portion of the total foulant mass.

The mass of the hard foulant layer was small compared to the slimy layer.
While  the buildup was  much less during  the second  six months of
operation, the mass of solids deposited was reduced substantially during
both periods by the regular in situ treatments with the HC1 gas.

The results of analyses conducted on the foulant samples taken from the
membrane tube diffusers  are summarized in Table 19. The foulant
samples collected during November 1986 were chosen by visually
selecting a representative area on the diffusers. Because of the geometry
of the tube diffusers, samples from the top and bottom of the units were
collected and analyzed in July 1987. The November results indicate
substantial differences in  the fouling of the membrane and ceramic
diffusers. The mass deposited on the membranes was much less than on
the ceramics, while the volatile fraction was higher and the acid soluble
fraction was equivalent The differences are explained by the results of
the analyses of the top and  bottom foulant samples. The mass of foulant
material makingup the outer slimy layer was not evenly distributed. Most
of the mass was on the top of the diffuser. The top portion of the foulant
is very similar to the foulant found on the ceramic diffusers indicating
that the fouling mechanisms for the top of the membranes and the
ceramics are similar.

The foulant material collected from the bottom of the  diffusers had much
less mass per unit area,  much higher volatile fractions and  lower acid
                         54

-------









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soluble fractions. These differences indicate that gravity settling may
play a role in the deposition of inert solids in the slimy foulant layer.
Removal of the inert solids before they reach the aeration basins could
possibly reduce the mass of foulant that builds up on the top surfaces of
the diffusers. The clean water oxygen transfer efficiency tests conducted
on the ceramic diffusers before and after hosing (refer to Tables 12 and
13) showed that the slimy foulant layer was responsible for most of the
losses in oxygen transfer efficiency. Since removing the inert solids may
reduce the total mass of foulant deposited, there is reason to believe that
the rate  at which  the overall system  efficiency  decreases would be
reduced too.

Cost Analysis

To  compare the sparged turbine, ceramic disc  and membrane tube
aeration systems, the capital, and the operation and maintenance (O &
M) costs were put on a common basis comprising treatment of 55 million
Ib BODs per year (150,700 Ib/day), approximately the average plant
loading from 1983 through 1985. The costs were also adjusted to reflect
the hypothetical situation in which all four quadrants have  the same
aeration system. This situation is used  for the cost analysis because it
provides a more equitable evaluation of the capital costs such as the acid
gas feed facilities which are the same for one or four quadrants.

Capital

The capital costs for the two fine pore diffuser  aeration systems are
summarized in Table 20. The capital costs shown for the retrofit of one
quadrant are the 1985 construction costs determined by competitive
bidding. The original bid included the fine pore aeration systems, the in-
line air filter for the ceramic diffuser system and the numerous pilot
headers provided for the comparative study. The acid gas storage and
feed building and the acid feed equipment were added to the original
contract by change order. The 1985 construction costs were not escalated
because prices have not risen appreciably over the last few years and
because the original construction package included extra features such
as the numerous pilot headers which would not be needed in the retrofit
of the remaining quadrants. In addition,  the  competitiveness among
manufacturers of  fine pore aeration  equipment has  increased. To
provide some factor of conservativeness, twenty percent was added to
the estimated  1988 construction costs  to cover engineering and
contingencies.

For the ceramic diffuser system, it was assumed that additional in-line
air  filters or a central filtration  system  located at the  inlet to the
compressors would not be necessary. Four  ceramic diffusers were


                        57

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 Table 20 - Summary of Capital Costs
                                       One             Four
 Component   	Quadrant	Quadrants
 Ceramic Discs
 Aeration System                    $386,400       $1,545,600
 Air Filtration                        101,300           ..     Q
 Acid Gas Feed Building               68,900           68,900
 Gas Cleaning Royalty2               ' 59,200          236*800
 Subtotal                            615,800        1,851,300
 Engineering & Contingencies         44,5003         370,3004
 Total                              $660,300       $2,221,600

 Membrane Tubes
 Aeration System                    $416,300       $1,665,200
 Engineering & Contingencies          44,5003        333,Q004
  Total                             $ 460,800       $ 1,998,200

 1 Based on Contractor's 1985 Schedule of Values plus change orders.
 2 U.S. Patent No. 4,382,867 held by Water Pollution Control Corporation, Milwaukee
 Wisconsin 53201.
 3 One-half of the actual engineering design and construction fees.
 4 Engineering and contingencies estimated at 20 percent of construction.
installed on a pilot header provided  by the ASCE for an inter-plant
fouling study. The ASCE header was placed in quadrant 4 and was fed
air that  did not pass through the in-line filter. After approximately 16
months of operation, there was no sign of air-side fouling based on BRVs
measured on the air side of the diffusers.

The air diffusion equipment cost estimate for the ceramic disc fine pore
diffuser system was about $ 120,000 less than the membrane tube diffuser
system. Even with the  additional cost for the acid gas feed facilities, the
ceramic system was about $50,000 less. The cost item that calces the
ceramic system more expensive was the royalty paid for practicing the in
situ acid gas cleaning system. To clean all the diffusers in both the contact
and reaeration basins would cost nearly a quarter of a million dollars.

Operation

The costs for operation of the two fine pore aeration  systems and the
sparged turbine aeration system include the labor for process monitoring
and adjustment of the activated sludge control parameters,  and the
electrical power to run the air compressors and the turbine mixers. Since
all three aeration systems require an  equivalent amount of effort for
                         58

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monitoring the activated sludge process and adjusting the air flow rate
to the basins, the costs were not included in the comparison.

A comparison of the electrical power usage before and after the two
quadrants were retrofitted with the fine pore diffusers is presented in
Table 21. In the years 1983,1984 and 1985, the sparged turbine aeration
system was used exclusively. The average annual electrical power usage
was 25.8 million kilowatt-hours (KWH)  and the cost was $1,032,200
($0.04/KWH). The average unit cost was $18.56/1000 Ib BODs treated.
In comparison, the power usage during the first 12 months of operation
with the two quadrants of fine pore diffusers (and usually one sparged
turbine contact basin) was 18.0 million KWH at an total cost of $721,000.
The unit cost was $12.42/1000 Ib BODs treated. This was a reduction in
electrical power usage of 7.8 million KWH for a savings of $311,200 or
30 percent less than the three-year average of sparged turbine operation.
Based on the unit costs, the reduction was slightly greater at 33 percent
($12.42 versus $18.56/1000 Ib BODs treated) because more BODs was
treated during the first 12 months of the study period. The last six months
of the study period were not included in the comparison because the
BODs loading to the plant was substantially lower and at least for part
of the period, the activated sludge system was in an upset condition.

The electrical power usage and cost for each of the two fine pore aeration
systems were estimated based on the air volumes used. The sum of the
monthly average contact and reaeration basin air flow rates were
converted to electrical power usage as follows:

      P = Q (0.032) (24) (N)

Where:

      P = monthly average power usage, KWH/month

      Q = monthly average air flow rate to the quadrant, scfm

      0.032 = kilowatts per scfm at a discharge pressure of 9.5 psig
              taken from the 1984 compressor test report7, KW/scfm

      24 = hours/day

      N = number of days operated during the month, day/month
The power used to compress air for operation of the quadrant with the
sparged turbines was calculated as the difference between the usage for
the fine pore systems and the total billed amount for the month taken
from GBMSD records. Using this method essentially assigned all of the
                        59

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Table 21 - Electrical Power Usage and Cost Summary
Parameter Mixers Compressors
1983 (56.8 x 106 !b BOD5 treated)
Usage, KWH 10.8 x 10* 13.4 x 106
Cost,$ 432,400 . 537,000
$71000 Ib BODs 7.61 9.45
1984 (58.4 Ib x 106 BODs treated)
Usage, KWH 1 1.9 x 106 16.6 x 106
Cost, $ 477,800 665,200
$71000 Ib BODs 8.18 11.39
1985 (51.6 x 106 Ib BOD5 treated)
Usage, KWH 10.5 x 106 14.1 x 106
Cost, $ 419,000 564,900
$71000 Ib BODs 8.12 10.95
Average 1983 - 1985 (55.6 x 106 Ib BODs/year treated)
Usage, KWH 1 1. 1 x 106 14.7 x 10*
Cost,$ 443,200 589,000
$71000 Ib BODs 7.97 10.59
5/86 - 4/87 (58.1 x 106 Ib BODs treated)
Usage, KWH 3.6 x 106 14.4 x 106
Cost, $ 144,600 577,100
$71000 Ib BODs 2.49 9.93

Total
24.2 xlO6
969,000
17.06
28.5 x 106
1,143,000
19.57
24.6 x 106
984,400
19.07
25.8 x 106
1,032,200
18.56
18.0 xlO6
721,000
12.42
Note: Average cost per kilowatt-hour from 1983 through 1987 was S0.04/KWH. ',
 air fed to the reaeration basins to the fine pore systems although for most
 of the study one of the reaeration basins provided return activated sludge
 to both a fine pore diffuser equipped contact basin and a sparged turbine
 equipped contact basin.

 The power costs were calculated from the usage data using the rate of
 $0.04/KWH. Because the quadrants did not treat an equal quantity of
 BODs each month, the cost data were normalized by dividing the total
 cost by the pounds of BODs treated. The electrical power usage and cost
 data are tabulated in Appendix D.

. The power costs  per unit of BODs treated are plotted versus time in
 Figure 21. The ceramic diffusers provided more economical treatment
 than the membrane  diffusers in May 1986. After the first  month,
                         60

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00

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          CVJ
                    a co
                    CO 00

                    w o>

                    •2 *~

                    0) CO
                    O) CD
                    CO C
                     a
                                   •P
                                   /
                           a
                              a
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-------
however,  the  oxygen transfer efficiency of the ceramic diffusers
decreased resulting in higher operating costs compared to the membrane
diffusers. No further increase in treatment cost was experienced after the
third month of operation. During the same initial six months of
operation, the membrane diffusers showed more variation but no
increasing or decreasing trend in power costs. During the first six months
of operation, the membrane diffusers had lower unit power costs than
the ceramic diffusers, $10.64 versus $11.73/1000 Ib  BOD5 treated,
respectively.

After cleaning in November 1986, the cost of operating the ceramic
diffusers was reduced to the May 1986 level, approximately $9.00/1000
Ib BODs treated. Cleaning the membrane diffusers also resulted in a
decrease in the unit power costs to about $9.00/1000 Ib BODs treated.
Between December 1986 and the end of April 1987, the two fine pore
diffuser systems operated at equivalent unit costs. Not including the
February  1987 value for the membrane diffuser system, which is
considered an outlier (see discussion of efficiency factors), the average
unit power costs for the ceramic and membrane diffuser systems were
$9.95 and $9.66/1000 Ib BODs treated, respectively.

In May 1987, the activated sludge system was upset so the air flow rates
were not a good indicator of the electrical power actually required to
treat the incoming BODs. By the middle of June, the activated sludge
system had recovered but the efficiency of the fine pore aeration systems
was low and the energy usage was high so the diffusers were cleaned. The
membranes were cleaned the last week in June and the ceramics were
cleaned in July.

After cleaning, the power costs for the ceramics were again reduced to
the original like-new condition. The average unit power cost for the last
three months of the study was $9.64 /lOOO Ib BODs treated. The unit
power costs for the membranes after cleaning were reduced but not to a
like-new condition. The unit power costs remained  high,  averaging
$15.40/1000 Ib BODs for the last four months of  the study.  The
substantially higher unit power costs for the membranes are consistent
with the losses in oxygen transfer efficiency measured during the clean
water  oxygen  transfer efficiency testing done on the pilot and  grid
diffusers, as well as the measured air requirement per Ib of BODs in the
membrane quadrant

Maintenance

The annual average maintenance costs for the sparged turbine and the
two fine pore diffuser aeration systems are summarized in Table 22. The
costs are based on having all four quadrants equipped with the same


                         62

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 Table 22 - Estimated Maintenance Costs
 Aeration                                                      Estimated
 System	Maintenance Item/Activity	    Annual Cost
 Sparged        Compressors	  . $ 5,400
 Turbines       Turbine Mixers	    51*600
                   Total   •  •  •	$57^000

 Ceramic        Compressors   	      $5 490
 Discs           Diffusers:
                1) Drain contact and reaeration basins twice annually
                 and clean the diffusers
                   a) Labor (hosing) - 24 hours/quadrant/cleaning
                     @$30/hour    	$5,800
                   b) Labor (HC1 gassing) - 16 hours/quadrant/cleaning
                     @$30/hour    .	  _ 35800
                   c) Chemicals - HC1 gas @ $0.20/diffuser/cleaning and '
                     33,104  diffusers   	13,200
                2) In situ acid gas treat reaeration basin
                 diffusers monthly2
                   a) Labor - 6 hours/quadrant/cleaning @ $30/hour   7,200
                   b) Chemicals - HC! gas @ $0.20/diffuser/cleaning   ''
                    and 8,592 diffusers1	17,200

                   Diffuser subtotal	$47,200

                   Total	$52,600

 Membrane     Compressors	 $ 8 100
Tubes         Diffusers:
                1) Drain contact and reaeration basins annually
                   and clean the diffusers
                   a) Labor - 72 hours/quadrant/cleaning              ,
                    @$30/hour	8,600
                   b) Supplies - none	  . 0
               2) Flexing not required	0

               Total	$ 16,700
 6,128 diffusers/contact basin and 2,148 diffusers/ reaeration basin.

 Ten monthly treatments/year in addition to the two treatments associated with the semi-annual
cleaning.
                                     63

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 aeration system. For the fine pore aeration systems, the basis is operation
 of all four quadrants, each quadrant having the same number of diffusers
 that were installed in the test quadrant.

 For the sparged turbines, the compressor and turbine maintenance costs
 are based on the data assembled and reported in the 1983 Predesign
 Report  escalated 5 percent per year to 1988.

 The compressor maintenance costs for the ceramic diffuser alternative
 are estimated to be equal to the sparged turbine alternative because the
 air usage for the two  types of equipment  are equivalent. The
 maintenance costs for the ceramic disc diffusers include draining each
 contact and reaeration basin twice annually for inspection and cleaning
 of the diffusers. The cleaning procedure comprises hosing the diffusers
 from the basin walkways using fire hoses followed by an in situ acid gas
 treatment immediately after the basin is put back into service. The labor
 estimate for hosing the diffusers is based on two operators for 8 hours
 each for a contact basin and 4 hours each for a reaeration basin. For the
 acid gas treatments, the estimate is for two operators for one half hour
 per grid. Monthly acid gas treatments are included for the reaeration
 basin diffusers to minimize the effects of the black foulant layer.

 The estimated compressor maintenance costs for the membrane tube
 diffuser alternative is based on the diffusers having the oxygen transfer
 efficiency measured at the end of the study when considerably more air
 was required. Since more than one compressor would be required at
 times to meet the additional air requirement,  the  maintenance costs
 would be higher. An increase of 50 percent was used for the estimate.
 When the  diffusers  were new and the air volume compressed was
 equivalent to that for the sparged turbines and the ceramic disc diffusers
 the compressor  maintenance costs  would be equal for all  three
 alternatives.

 Since cleaning of the membrane diffusers did not provide a substantial
 improvement in the oxygen transfer efficiency and the DWP of the
 fouled diffusers was not excessive, a minimal diffuser maintenance effort
 comprising an annual draining of the contact and reaeration basins for
 inspection and diffuser cleaning is used. The labor estimate is based on
 six operators working eight hours each to clean a contact basin and four
 hours to clean a reaeration basin. The cleaning procedure would be
 hosing from the basin floor and brushing with a stiff bristled scrub brush.
 Flexing of the membranes is not necessary.

The sparged turbines have the highest estimated annual maintenance
costs at $57,000, followed by the ceramic disc diffusers at $52,600 and
the membrane tube diffusers at $16,700.
                         64

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               Summary
               The estimated capital and annual O & M costs are summarized in Table
               23. The unit power cost for the turbines is based on the average for the
               period from 1983 through 1985. A unit cost of $10.00/1000 Ib of BODs
               treated was used for the ceramic system because it appears to be a
               reasonable estimate for a 6-month run between diffuser cleaning. The
               average cost for the period from December 1986 through April 1987, a
               5-month period, was $9.95/1000 Ib of BODs treated and  for the period
               from  August 1987 through October  1987, a 3-month period, was
               $9.64/1000 Ib of BODs treated. The unit cost of $15.40/1000 Ib of BODs
               treated was used for the membranes. This was the average cost associated
               with the last four months of the study.

               The ceramic disc diffuser system is estimated to save about $471,000 per
               year in electrical power costs and a total of $475,000 per year in total O
               & M costs compared to the sparged turbine aeration system. The payback
               on the capital investment would be about four and a half years.

               The membrane tube diffusers would have shown similar economics had
               they not lost their initial high efficiency. Based on the new diffusers, the
               annual savings in total O & M costs are estimated at $514,000 which
Table 23 - Alternative Aeration Systems Cost Summary
Cost Parameter
Sparged     Ceramic        Membrane Tubes
Turbines	Discs        New        Used
                                     0  $2,221,600  $1,998,200   $1,998,200
                              1,020,800J
                                 57,000
                                     0
              550,000"
                5,400
               47,200
550,000"
  5,400
  8,600
Capital
Operation and Maintenance1
  Electrical Power2
  Mechanical Maintenance
  Diffuser Cleaning
  Total O&M

  O&M Present Worth6

Total Present Worth7


 Annual cost.
2 Based on treating 55 million Ib BOD5/year.
 Based on a unit power cost of $18,56/1000 Ib BODS treated.
 Based on a unit power cost of $10.00/1000 Ib BODS treated.
 Based on a unit power cost of $15.40/1000 Ib BODS treated.
 Present worth based on 20 years @ 8-7/8 percent interest, present worth factor = 921
 Capital + O&M Present Worth.
847,000-
  8,100
  8,600
                             $1,077,800   $  602,600  $  564,000   $  863,700

                             $9,927,500   $5,549,900  $5,194,400   $7,954,700

                             $9,927,500   $7,771,500  $7,192,600   $9,952,900
                                       65

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             would have provided a payback period of about four years. However, the
             lost transfer efficiency resulted in a substantial increase in the electrical
             power requirements and actual O & M savings of only $214,000 per year.
             The payback period under these circumstances would be more than nine
             years. Based on a 20- year life of the equipment and an interest rate of
             8-7/8 percent, retrofitting with the membrane tube diffusers would not
             be economical because the total present worth of the retrofit is greater
             than the cost of continuing to operate the sparged turbines.
CONCLUSIONS
             The activated sludge system at Green Bay provided a severe test for the
             ceramic disc and membrane tube diffuser systems. The fouling on both
             types of diffusers appeared to be exacerbated by the inert solids which
             probably entered the aeration basins with the mill wastewaters. The
             plasticized PVC membrane material appears to have been adversely
             affected by environmental conditions including the temperature of the
             mixed liquor, which had summer monthly averages above 85°F.

             In situ acid gas treatments of the ceramic diffusers and flexing of the
             membrane diffusers did not  control deposition of a  loosely attached
             slimy foulant layer which had a substantial adverse effect on oxygen
             transfer efficiency. The in situ acid gas treatments of the ceramic
             diffusers controlled increases in DWP in both the contact and reaeration
             basins, but especially in the reaeration basin  where an kon-orataining
             precipitate formed on the ceramic diffusers, resulting in a marked
             increase in backpressure.

             The oxygen  transfer efficiency and operating pressure of the ceramic
             diffusers could be restored to a like-new condition by draining the basins
             and cleaning the diffusers with a three-step procedure consisting of
             hosing from the walkways, acid gas injection, and rehosing. The
             maintenance procedure could be shortened without reducing the
             effectiveness of the cleaning if after the initial hosing, the basin was put
             back into service and the in situ acid gas treatment was performed
             immediately.

             After 10 months in operation, cleaning the membranes by hosing from
             the basin floor, scrubbing, and rehosing, reduced the operating pressure
             to values substantially below typical new membranes, but did not restore
             the oxygen transfer efficiency. The unrecoverable loss in oxygen transfer
             efficiency was  about 25 percent based on clean water  test results. Data
             from the full-scale operation indicated that the permanent loss may have
             been even greater.
                                      66

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             Retrofitting the Green Bay Metropolitan Sewerage District's aeration
             basins with fine pore diffusers was cost-effective. A capital investment
             of about $1 million resulted in a first year electrical power savings in
             excess of $300,000.

             Further savings would be expected if all the sparged turbine aerators
             were replaced with ceramic fine pore diffusers or membrane diffusers
             that did not lose oxygen transfer efficiency with use.

             The  oxygen transfer  efficiency of the ceramic diffusers could be
             increased by about  10 percent if the air flow rate per diffuser were
             reduced to the normal design rate of 1.0 to 1.25 scfm per unit from the
             over 2.0 scfm/unit operating rate used during most of the study. From an
             oxygen transfer efficiency standpoint, this could be best accomplished by
             retrofitting more basins with the fine pore diffusers and then operating
             all available basins.
RECOMMENDATIONS
             Based on the results of the 18-month evaluation of the two fine pore
             diffuser systems, it would be very economical for the GBMSD to retrofit
             quadrants 1 and 3 with ceramic fine pore diffusers. However, until the
             GBMSD completes their facility planning effort and a decision can be
             made regarding further retrofits, we recommend that the following
             interim activities be pursued:

             1. Continue to monitor the operation of the fine pore aeration systems
                to build a data base for operation on the wastewater that has been
                received since the mill changes encountered in May 1987. The ef-
                ficiency of the two aeration systems can be monitored by calculating
                efficiency factors (see Appendix A) and verifying the efficiency fac-
                tors by conducting infrequent off-gas analyses.

             2. Continue to in situ acid gas treat all the reaeration basin ceramic dif-
                fusers monthly to minimize buildup of the black foulant material.

             3. In situ acid gas treat one ceramic grid in the contact basin monthly to
                investigate if there is a long term benefit to providing regular treat-
                ments between draining of the basins for restorative cleaning.

             4. As an alternative to using gaseous HC1 as the second step in the res-
                torative cleaning procedure, try using liquid HC1. The procedure
                comprises three steps: hosing of the diffusers from the walkways, ap-
                plying  14 percent HC1 using  stainless steel spray applicators and
                rehose after 20 to 30 minutes. This method has proven to be effective
                in a number of plants. If handling of the liquid acid is not a problem,
                                      67

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  the cost of acid cleaning would be substantially reduced because the
  gas cleaning royalty would only have to be paid on diffusers installed
  in the reaeration basins.

5. Test one or more alternative membrane tube diffusers in the reaera-
  tion basin where one grid contains 233 difrusers. There are membrane
  diffusers available that have the 3/4 inch pipe thread connector now
  being used and are made of materials other than plasticized PVC. One
  of the alternative materials may provide the advantages experienced
  with the membrane difrusers but without the relatively rapid loss in
  oxygen transfer efficiency.

6. Continue to run unfiltered air through a few ceramic difrusers at 2 to
  3 cfm per unit and monitor the air-side BRV periodically to see if ad-
  ditional air filtration is needed in the final design.
                          68

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                                   REFERENCES


 1. Donohue & Associates, Inc., "Predesign and Feasibility Report for Aeration System
   Modifications", Report prepared for the Green Bay Metropolitan Sewerage District
   December 1983.                                                           ^

 2. Saiiitaire - Water Pollution Control Corporation, "Oxygen Transfer Shop Test Report,"
   Report prepared for the R. P. Honold Company, Sanitaire job no. 85-1206, September 1985.

 3. Parkson Corporation and Gerry Shell Environmental Engineers, Inc., "Oxygen Transfer
   Evaluation of the Wyss Flex-A-Tube Aeration System," Report prepared for the R.P. Honold
   Company, August 1985.

 4. Redmon, D.T., Boyle, W.C., Ewing, L., "Oxygen Transfer Efficiency Measurements Using
   Off-Gas Techniques," Journal WPCF, Vol. 55, No. 11, November 1983.

 5. Ewiing Engineering Company,  Inc., "Results of Off-Gas Testing at the Green Bay
   Metropolitan Sewerage District - May 1986 through October 1987," Report prepared for
   Donohue & Associates, Inc., June 1988.

 6. Allbaugh, T.A., Benoit, DJ., Spangler, J., "Aeration System design Using Off-Gas
   Oxygen  Transfer Testing," Paper presented at the 58th Annual Conference of the  Water
   Pollution Control Federation, October 6-10,1985, Kansas City, Missouri.

 7. Domohue & Associates, Inc., "Aeration System Predesign Test Program," Report prepared
   for the Green Bay Metropolitan Sewerage District, September  1984.

 8. Box, G.E.P., Hunter, W.G., and Hunter, J.S., Statistics for Experimenters - An
   Introduction to Design. Data Analysis, and Model Building, John Wiley & Sons, New York,
   A y I o*

9. Volk, W., Applied Statistics for Engineers. McGraw-Hill Book Company, New York, 1969.
                                           69

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               APPENDIX A
EFFICIENCY FACTOR CALCULATION DESCRIPTION
                   70

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                         APPENDIX A
                Efficiency Factor Calculation Description


Contact basin efficiency factors are calculated as follows:

     EF = BODs / Q. / FDO

Where:

     EF   = contact basin efficiency factor,  Ib BODo/day/cfro
            corrected to zero dissolved  oxygen concentration

     BODs = BODs loading to  the contact  basin, Ib/day

     Qm   = nominal air flow rate to the contact basin based
            on the computer  logged data,  cfm

     FDO  = dissolved oxygen correction  factor, decimal
            fraction
          = 
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Table Bl - Clean Water Dissolved Oxygen Saturation
           Concentrations as a Function of Time
Temperature
°F
67
68
69
70
71
72
73
74
75
76
77
78
Concentration
mg/1
3. 19
9.09
8.99
8.89
8.80
8.71
8.62
8.53
8.44
8.35
8.26
8.18
Temperature
op
79
80
81
82
83
84
85
86
87
88
89
9O
Concent r at i on
mg/1
8. 10
8.02
7.94
7.86
7.78
7.71
7.63
7.56
7.49
7.42
7.35
7.28
                             72

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             APPENDIX B
STATISTICAL REVIEW OF THE OFF-GAS TEST
               RESULTS
                   73

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                          APPENDIX B
               Statistical Review of the Off-Gas Test Results
CONTACT BASINS

The statistical  significance of the differences observed in
the basin  average alpha'-SOTE data was evaluated by analysis
of variance  and  the F test.B Differences in the average
alpha'-SOTE  data were considered significant if the
calculated variance ratios were greater than F at the 0.05
significance level,  i.e.,  the probability that the average
alpha'-SOTE  values are equal is less than 5 percent.

The analysis of  variance  test was performed on alpha'-SOTE'
values that  were calculated as follows:

     alpha'-SOTE'  = (alpha' -SOTEi ) (Fi )7'Fb

Where:

     alpha'-SOTE'  = local  value of alpha'-SOTE adjusted for
                     variations in the off-gas flux within the
                     bay,  decimal.
     alpha'-SOTEi  = local  value of alpha'-SOTE, decimal.
     Fi            = local  off-gas flux, scfm/sq ft.
     Fb            = bay average off-gas flux, scfm/sq ft.

Each bay comprises one-sixth of the aeration basin. Usually,
four local measurements were made in each bay. The one
exception  was December 1986 when the daylight hour were
1i mi ted.

The data were blocked using the six bays.  In this way, the
analysis of  variance can  test the significance of variations
among the  bays.

The alpha'-SOTE,  off-gas  flux,  alpha'-SOTE'  and various
parameter  averages are presented in Tables Cl through C9. The
tables were  prepared to provide the data necessary for
calculating  the  following  quantities needed to assemble an
analysis of  variance table for  each test.

1. Sum of  squares of deviations associated with the blocks
   (bays), SB.

     SB =  ink SUMi  CCY'i-Y' )*]

2. Sum of  squares of deviations associated with the
   treatments (aeration equipment),  ST.

     ST =  mn SUMt  C(Y't-Y')a3                        ;
                              74

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3. Sum of squares of deviations  associated with the
   interaction between the blocks and  the treatments, SI.

     SI = m SUMt SUMi C=]

4. Residual sum of squares, SR.

     SR = SUMt SUMi SUMj  CCY'tij-Y'ti>aD

Where:

     k     = number of treatments,  t = 2  aeration systems.
     m     = number of measurements in each treatment block,
             j = 4 alpha'—SOTE'  values per bay.
     n     = number of blocks, i  = 6 bays.
     Y'    = average of all measurements.
     Y'i   = average value for a bay,  usually comprising 8
             values, 4 from each  aeration basin.
     Y't   = average value for a treatment,  usually  :
             comprising 24 values,  4 values from each of 6
             bays.
     Y'ti  = average value for each bay within a treatment,
             usually comprising  4 values.
     Y'tij = individual alpha'—SOTE values,  usually 48 local
             measurements.

The analysis of variance  results for the  nine off-gas tests
are presented in Tables CIO through CIS.  The results are
summarized as follows:

                  Significance of Differences @ O.05 Level
Test Date
5-13-86
5-15-86
7-02-86
7-3O-86
1O-3O-86
12-O3-86
6-18-87
8-05-87
10-28-87
Between
Aeration
Systems
No
No
No
No
No
No
No
Yes
Yes
Among
Bays
Yes
No
Yes
Yes
Yes
No
Yes
No
No
Interactions
No
No ;
No
No
No
No
No
No
No
                               75

-------
The analysis of variance indicates  that,, except for the last
two tests, the differences  in  the average alpha'-SOTE'  values
for the two aeration systems were not  significant although
many of the differences were more than 10 percent of the two
basin mean value. Collecting alpha*-SOTE data at  more
locations could have increased the  sensitivity of the
analysis of variance test by increasing the number of degrees
of freedom for the residual sum of  squares.  This  is a moot
point, however, because it  was not  practical  to sample more
than 48 positions in one day.

To test the adequacy of the 24 position per  basin sampling
plan, the 24 positions were divided into two data sets of 12
measurements consisting of  alternate north and south grids.
For example, the two sets for  contact  basin 2 are:

               Set No. 1            Set No.  2
                C2.ISA      ,    .     C2. 1NA .   .      ;.
                C2.1SB               C2.1NB
                C2.2NA               C2.2SA
                C2.2NB               C2.2SB
                C2.3SA               C2.3NA
                C2.3SB               C2.3NB
                C2.4NA               C2.4SA
                C2.4NB               C2.4SB
                C2.5SA               C2.5NA
                C2.5SB               C2.5NB
                C2.6NA               C2.6SA
                C2.6NB               C2.6SB

Similar sets were made from the contact  basin  4 data.  Once
again, alpha'-SQTE' data were used.  The December 1986  test
data were not used.

Two estimates of the basin average alpha'-SOTE'  were
calculated for each of the contact basins  from the data sets.
The two estimates were then evaluated using  a  t test on the
data pairs.* The data and the results of the t  test are
presented in Table C19. The t test indicates that  the  two
estimates of the basin average alpha'-SOTE'  were not
significantly different at the O.O5  significance level.  Since
both of the 12-position estimates provide  statistically
equivalent results,, it can be concluded  that the 24-position
sampling plan would provide a more precise estimate. Also,
the 12-position test conducted in December should  be
considered statistically sound.
                               76

-------
REAERATION BASINS

The alpha'-SOTE data for the reaeration  basins were evaluated
using the t test. The data were  not  blocked  because visual
inspection did not produce any indication  of systematic
spatial variations. The results  of the t tests are presented
in Table C20. The statistical tests  indicate that  differences
in the basin averages which are  greater  than 6 percent of  the
two basin mean were significantly different  at the O.O5
significance level.
                               77

-------
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-------
            Table CIO - ANALYSIS OF VARIANCE TABLE - Test  Conducted on  13 Nay  1386

Source of    Sui of             Degrees of            Mean Square          Ratio of
Variation    Squares (SS>       Freedoi (D.F.)        (SS/D.F.)            Mean Squares                F(0.05,D.F.n,D.F.d)
Blocks       SB =  0.0184       n-1 = 5                S'B = 0.0037         S'B/S'e =    2.9066        F(0.05,5,36) = 2.48
(Bays)

Treatients   ST =  0.0034       k-1 = 1                S»T = 0.0034         S'T/S'e =    2.6583        F(0.05,l,36) = 4.11
(Equipment)

Interaction  SI =  0.0024       (n-D*                 S11 = 0.0005         S'l/S'e =    0.3862        F(0.05,5,36) = 2.48
                                  (k-1) =5                                                                               :

Error        Se =  0.0455       nk(r-l) =36           S'e = 0.0013


Total        S  =  0.0697        N - 1 = 47                                                       ;                        ;

            NOTE:
            k = Nuiber of treatments, i.e., tvo types of fine pore diffusers
            • = Nuiber of replicates, i.e., four saipling positions  per  bay
            n = Nuiber of blocks, i.e., six bays
            N = Total nuiber of leasureients

         •  If the Ratio of Mean Squares is > F(0.05,D.F.n,D.F.d), the hypothesis of equal variances is rejected and
            the leans are considered significantly different at the  0.05 significance  level.
                                                        87

-------
            Table Cll - ANALYSIS OF VARIANCE TABLE - Test  Conducted on 15 Hay 1986
Source of
Variation
Blocks
(Bays)
Treatments
(Equiptent)
Interaction
Error
Sui of
Squares
SB = 0
ST = 0
SI = 0
Se = 0
(SS)
.0147
.0015
.0032
.0446
Degrees of
Freedoi (D.F.)
n-1 = 5
k-1 = 1
(n-l)t
(k-1) = 5
nkd-1) = 36
Mean Square
(SS/D.F.)
S'B = 0.0029
S'T = 0.0015
S'l * 0.0006
S'e = 0.0012
Ratio of !
Hean Squares F(0.05,D.F.n,D.F.d) ;
S'B/S'e = 2.3797 F(0.05,5,36) = 2.48
S'T/S'e = 1.2489 i F(0.05,l,36) = 4.11 ,
S'l/S'e = 0.5122 ' F(0.05,5,36) = 2.48 ;
.
Total        S  =  0.0640        N - 1 = 47

            MOTE:
            It = Nuiber of treatients,  i.e., tvo types of fine pore diffusers
            • = Nuiber of replicates,  i.e., four saipling positions per bay
            n = Nuiber of blocks, i.e., six bays                                                   ;
            IN = Total nuiber of leasureients

            If the Ratio of Mean Squares is > F(0.05,D.F.n,D.F.d), the hypothesis of equal  variances is rejected and
            the leans are considered significantly different at the 0.05 significance level.

-------
            Table C12 - ANALYSIS OF VARIANCE TABLE - Test  Conducted  on 2 July  1986

Source of    Sui of             Degrees of            Mean Square          Ratio of
Variation    Squares (SS)       Freedot (D.F.)         (SS/D.F.)            Hean Squares                F(0.05,D.F.n,D,F.d>
Blocks       SB =  0.0962       n-1 = 5                S'B =  0.0192         S'B/S'e =     3.5394        F(0.05,5,36) = 2.48'
(Bays)                                                                                                                   i
                                                                                                                         !

Treatments   ST =  0.0019       lc-1 = 1                S'T =  0.0019         S'T/S'e =     0.3585    '    FCO.05,1,36) = 4.11:
(Equipment)                                                                                                              ;

Interaction  SI =  0.0088       (n-D*                 S'I =  0.0018         S'l/S'e =     0.3250        F(0.05,5,36) = 2.48
                                  (k-1) =5

Error        Se =  0.1957       nkd-1) = 36           S'e =  0.0054


Total        S  =  0.3027        N - 1 = 47

            NOTE:                                                                                                        i
            k = Nuiber of treatients,  i.e., t«o  types  of  fine pore diffusers                                              '
            • = Nuiber of replicates,  i.e., four saipling  positions per bay
            in = Nuiber of blocks,  i.e., six bays                                                  >
            N = Total nuiber of teasureients

            If the Ratio of Hean Squares is > F(0.05,D.F.n,D.F.d), the hypothesis of equal variances is rejected and
            the leans are considered significantly different  at  the 0.05 significance level.
                                                       89

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            Table C13 - ANALYSIS OF VARIANCE TABLE - Test Conducted on 30 July  1986

Source of    Sui of             Degrees of            Mean  Square          Ratio of
Variation    Squares (SS)        Freedoi (D.F.)        (SS/D.F.)            Hean Squares                F(0.05,D.F.n,D.F.d):
Blocks       SB =  0.0286       n-1 = 5                S'B = 0.0057         S'B/S'e =    2.7473        F(0.05,5,36) = 2.48
(Bays)

Treatments   ST =  0.0074       k-1 = 1                S'T = 0.0074         S'T/S'e =    3.5291        F(0.05,l,36) = 4.11
(Equipment).

Interaction  SI =  0.0034       (n-D*                 S'I = 0.0007         S'l/S'e =    0.3281        F(0.05,5,36) = 2.48;
                                  (k-1)'=5                                                                               ;

Error        Se =  0.0750       nkd-1)  =  36           S'e = 0.0021


Total        S  = .0.1144        N -  1 = 47

            MOTE:                                                                                 ;
            k = Nuiber of treatients, i.e., two types  of  fine  pore diffusers                       :
            • = Nuiber of replicates, i.e.,  four  saipling positions  per  bay
            n - Nuiber of blocks,  i.e.,  six bays                                                   :
            i - Total nuiber of teasureients

            If the Ratio of Mean Squares is  >  F(0.05,D.F.n,D.F.d), the hypothesis of equal variances  is rejected and      i
            the leans are considered  significantly different at the  0.05 significance  level.
                                                            90

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Table C14 - ANALYSIS OF VARIANCE TABLE - Test  Conducted on 30 October 1986
Source of
Variation
Blocks
(Bays)
Treat lent s
(Equipient)
Interaction

Error
Total

iiui of
Squares (SS)
!>B = 0.0181

!5T = 0.0031
i •
SI = 0.0098

Se = 0.0480
S = 0.0791
NOTE:
Degrees of
Freedoi (D.F.)
n-1 = 5

k-1 = 1

(n-D*
(k-1) = 5
nkd-1) = 36
N - 1 = 47

Mean Square
(SS/D.F.)
S'B = 0.0036

S'T = 0.0031

S'l = 0.0020

S'e = 0.0013


Ratio of
Hean Squares F(0.05,D.F.n,D.F.d)
S'B/S'e = 2.7219 F(0.05,5,36) = 2.48

S'T/S'e = 2.3542 F(0.05,l,36) = 4.11

S'I/S'e= 1.4744 F(0.05,5,36) = 2.48




k = Nuiber of treatments, i.e., tvo types of fine pore diffusers
• - Nuiber of replicates, i.e., four saipling positions per bay
n = Nutber of blocks, i.e., six bays
N = Total nuiber of leasureients

If the Ratio of Mean Squares is > F(0.05,D.F.n,D.F.d), the hypothesis of equal variances is rejected and
the leans are considered significantly different at the 0.05 significance level.
                                                91

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            Table CIS - ANALYSIS OF VARIANCE TABLE - Test Conducted on 3 Deceiber 1986                                   ;

Source of    Sui of             Degrees of            Mean Square          Ratio of                                      !
Variation    Squares (SS)       Freedoi (D.F.)        (SS/D.F.)            Mean Squares               F(0.05,D.F.n,D.F.d)
Blocks       SB =  0.0213       n-1 = 5                S'B = 0.0043         S'B/S'e =    0.8926       F(0.05,5,12) = 2.48
(Bays)                                                                                                                   '

Treatients   ST =  0.0045       k-1 = 1                S'T = 0.0045         S'T/S'e =    0.9388       F(0.05,l,12) = 4.1l!
(Equipment)

Interaction  SI =  0.0047       (n-l)t                 S'I = 0.0009         S'l/S'e =    0.1975  ;     F(0.05,5,12) = 2.48


Error        Se =  0.0572       nkd-1) = 12           S'e = 0.0048


Total        S  =  0.0877        N - 1 = 47                                                       •                       ;
                                                                                                 P                        i
            NOTE:
            k = Nuiber of treatments, i.e., tvo types of fine pore diffusers
            m = Nuiber of replicates, i.e., four saipling positions per bay
            n = Number of blocks, i.e., six bays
            N - Total number of measureients

            If the Ratio of Mean Squares is > F(0.05,D.F.n,D.F.d), the hypothesis of,equal  variances  is rejected and
            the means are considered significantly different at the 0.05 significance level.
                                                             92

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            Table CIS'- ANALYSIS OF VARIANCE TABLE - Test Conducted on 18 June  1987

Source of    Sui of             Degrees of            Mean Square          Ratio  of                I
Variation    Squares (SS)       Freedoi (D.F.)        (SS/D.F.)             Mean Squares                F(0.05,D.F.n,D.F.d)
Blocks       SB =  0.0255       n-1 = 5                S'B = 0.0051         S'B/S'e =    4.4108        F(0.05,5,36) = 2.48
(Bays)

Treatments   ST =  0.0002       k-i = 1                S'T = 0.0002         S'T/S'e =    0.1757        F(0.05,l,36) = 4.11
(Equipient)                                                                                                              •

Interaction  SI =  0.0005       (n-D*                 S'I = 0.0001         S'l/S'e =    0.0893        F(0.05,5,36) = 2.48
                                  (k-1) = 5

Error        Se =  0.0417       nkd-1) = 36           S'e = 0.0012


Total        S  =  0.0679        N - 1 = 47                                                       ;                       ;

            NOTE:
            k = Nuiber of treatients, i.e., two types of fine pore diffusers                                             •
            • = Nuiber of replicates, i.e., four sampling positions per bay
            n = Nuiber of blocks, i.e., six bays
            N = Total nuiber of leasureients

            If the Ratio of Mean Squares is > F(0.05,D.F.n,D.F.d), the hypothesis  of equal variances is rejected and
            the leans are considered significantly different at the 0.05 significance  level.
                                                           93

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             Table C17 - ANALYSIS  OF  VARIANCE TABLE - Test Conducted on 5 August 1987

 Source of    Sui of            Degrees of            Mean Square          Ratio of

 !!-™!"    SqUareS  (SS>       Freed°' (D  ST=  °'1238       k"1 = I          S     S'T = 0.1298         S'T/S'e  =    21.3557        FCO.05,1,36) M.ll


 Interaction  SI =  0.0166       (n-l)*_              S' I = 0.0033         S'l/S'e  =     0.5471        F(0.05,5,36) = 2.48
                                  vK~U ~ 0

Error        Se =  0.2189       nk(t-l) = 36           S'e = 0.0061                               ,


Total        S  =  0.4128        N - 1  = 47

            HOTE:
            I: = Nuiber of treatments, i.e.,  two  types of fine pore  diffusers                                               '.
            n = Nmber of replicates, i.e.,  four saipling  positions per bay
            n = Nuiber of blocks,  i.e.,  six  bays                                               •   '                        ;
            M = Total number of  leasureients                                                                              ,'

            If  the Ratio of Hean Squares  is  > F(0.05,D.F.n,D.F.d),  the hypothesis of  equal variances is rejected and
            the leans are considered significantly different  at the 0.05 significance level.
                                                         94

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            Table CIS - ANALYSIS OF VARIANCE TABLE - Test  Conducted on  28  October  1987
Source of    Sui of             Degrees of
Variation    Squares (SS)       Freedom (D.F.)

Blocks       SB =  0.0273       n-1 =5
(Bays)
                  f

Treatients   ST =  0.0410       k-1 = 1
(Equipient)

Interaction  SI =  0.0056       (n-D*
                                  (k-1) = 5
Error
Se =  0.1049       nk(i-l) = 36
                                        Mean Square
                                        (SS/D.F.)

                                         S'B =  0.0055
S'T = 0.0410


S'l = 0.0011


S'e = 0.0029
                    Ratio of
                    Mean Squares
                     S'B/S'e =     1.8711
                                                              S'T/S'e =    14.0616
                                                              S'l/S'e =     0.3872
F(0.05,D.F.n,D.F.d)

F(0.05,5,36) = 2.48


F(0.05,l,36) = 4.11


F(0.05,5,36) = 2.48
Total        S  =  0.1787        H - 1  =  47

            NOTE:
            k = Ninber of treatients, i.e.,  two types of  fine pore diffusers
            • = Nuiber of replicates, i.e.,  four  sampling positions per bay
            n = Nuiber of blocks,  i.e., six  bays
            N = Total nuiber of teasureients

            If the Ratio of dean Squares  is  > F(0.05,D.F.n,D.F.d), the hypothesis of equal variances is rejected and
            the leans are considered significantly different at  the 0.05 significance level.
                                                         95

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                Table C19 - Analysis of Two 12-Position Saipling Plans

                    Contact Basin 2 - Ceraiics                 Contact Basin 4 - Membranes
Alpha' -SOTE'
Est. 1 Est. 2
5-13-86
5-15-86
7-02-86
7-30-86
10-30-86
12-03-86
6-18-87
8-05-87
10-28-87
0.1548
0.1552
0.1811
0.0977
0.1254
Insufficient
0.1098
0.2160
0.1807
0.1375
0.1425
0.1813
0.0936
0.1206
data
0.1182
0.2310
0.1622
Diff.
2 - 1
-0.0173
-0.0127
0.0002
-0.0041
-0.0048

0.0084
0.0150
-0.0185
Alpha'
Est. 1
0.1655
0.1584
0.1689
0.1189
0.1492

0.1075
0.1214
0.1083
-SOTE'
Est. 2
0.1609
0.1620
0.1680
0.1221
0.1291

0.1122
0.1175 .
0.1178
Diff.
2 - 1
-0.0046
0.0036
-0.0009
0.0032
-0.0201

0.0047
-0.0039
0.0095
Note:    Data froi Tables Cl through C9.
         Est, 1  comprises data froi positions ISA,  1SB, 2NA, 2NB, 3SA, 3SB, 4NA,  4KB,  5SA,  5SA, 6NA,  6NB.
         Est. 2  cotprises data fro§ positions 1NA,  1NB, 2SA, 2S8, SNA, 3NB, 4SA,  4SB,  SNA,  5NB, 6SA,  6S8.

                t Test (reference 9)
                Mean difference of all 16 pairs of  data, d'  = - 0.0026
                Standard deviation of the differences,  s'(d) =   0.0103
                t = !d'!/£s'(d)/(n)«0.5] = 0.0037/10.01/4]  =   0.064
                t(0.05,15) = 2.15
                Since t < t(0.05,15), accept null hypothesis that the two leans  are  equal.
                                                           96

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Table C20 - Statistical  Analysis of  Reaeration Basin Alpha'-SOTE Data  (t test)
fiuad.
5-12-86 82
84
Oiff.
5-16-86 82
84
Oiff.
7-01-B6 62
84
Diff.
7-29-86 82
84
Diff.
10-29-86 82
84
Oiff.
12-02-86 62
84
Diff.
6-17-87 82
84
Diff.
8-04-87 62
84
Diff.
10-27-87 82
84
Alpha'
-SOTE
0.1822
0.1757
0.0065
0.1696
0.1697
-0.0001
0.2118
0.1838
0.0280
0.1426
0.1122
0.0304
0.1155
0.1336
-0.0181
0.1955
0.1310
0.0645
0.1178
0.1108
0.0070
0.2321
0.1365
0.0956
0.1953
0.1268
S(I>
0.0219
0.0204

0.0138
0.0168

0.0173
0.0290

0.0164
0.0271

0.0092
0.0157

0.0194
0.0113

0.0127
0.0075

0.0406
0.0150

0.0212
0.0216
U0.05,
D.F. s'd) D.F.p t D.F.p) Result
11 0.0212 22 7.975 2.074 SO r
H . !

11 0.0154 22 0.016 2.074 USD •
11 ! ' !

11 0.0239 22 2.872 2.074 SD
11

11 0.0224 22 3.325 2.074 SD !
H ;

11 0.0129 22 3.446 2.074 SD ;
11

9 0.0159 18 9.071 2.101 SD
9 ;

11 0.0104 22 1.644 2.074 USD
11 ; i
!
11 0.0306 -22 7.651 '• 2.074 SD •
11

11 0.0153 22 10.986 2.074 SD
11
Oiff.   0.0685                                                                  ,

s(x)        = standard deviation of  the teasureients
D.F.        = degrees of freedoi for each set of  basin •easureients
s'(x)       = pooled estiiate of the standard deviation of all leasuretents
D.F.p       = degrees of freedoi for the pooled estitate  of  the standard deviation
t           = !x'i-x'2!/[s'(x)(l/nl+l/n2)«0.5J
t(0.05,Ofp) = value of t for probability of 0.05  and  D.F.p degrees of freedoi
Result      = if t > t(0.05,DFp) then the leans are significantly different (SD)
            = if t < t(0.05,DFp) then the leans are not significantly different (NSD)
                                             97

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           APPENDIX C
OPERATIONAL COST DATA SUMMARIES
               98

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