United States
                Environmental Protection
                Agency
Risk Reduction
Engineering Laboratory
Cincinnati, OH 45268
                Research and Development
EPA/600/SR-92/114  October 1992
EPA       Project Summary
                Modifications to  Reduce  Drag
                Out  at a Printed  Circuit  Board
                Manufacturer
                Teresa M. Harten and Paul E. Pagel
                  The waste reduction capabilities of
                two simple, drag-out-reducing modifi-
                cations were demonstrated at a Minne-
                apolis-area,  printed  circuit board
                manufacturer  in an evaluation per-
                formed under the Minnesota/U.S. Envi-
                ronmental  Protection  Agency  (EPA)
                Waste Reduction Innovative Technol-
                ogy Evaluation (WRITE) Program. The
                low (or  no)  cost,  low technology
                changes made  were (1) slowing  the
                withdrawal  rate of racks containing the
                printed circuit boards as they were
                pulled from an etchant process tank
                and an electroless copper process tank
                and (2)  combining  an  intermediate
                withdrawal  rate with a longer drain time
                over the process tanks. Both modifica-
                tions significantly reduced drag out of
                concentrated, copper-containing bath
                solutions into the rinse water systems.
                  The first  modification reduced drag
                out by 45% for the etchant  bath and
                50% for  the electroless  copper bath.
                When compared with the baseline, the
                second modification reduced drag  out
                by 41% for the etchant bath and 52%
                for the electroless copper bath. By re-
                ducing drag out in these amounts, 203
                and 189 g of copper per day were  not
                discharged as waste in the rinse water
                waste stream for modifications 1 and
                2, respectively.  Because copper con-
                centration in rinse water was reduced,
                the  potential for conserving rinse wa-
                ter flows was also shown, although this
                was not directly tested.
                  The  total potential  annual  savings
                was calculated at $3350 for the first
                modification and $3120 for the second
                modification. For the first modification,
                $2640 was saved in treatment and dis-
                posal costs and the remainder, $710,
was the projected savings in water and
sewer  charges because rinse water
could be reduced proportionate to drag
out reduction. The same figures for the
second modification were $2460  and
$660, respectively. Since no capital
costs were  incurred in making  the
changes, payback would  be immediate.
  This Project Summary was developed
by EPA's Risk Reduction Engineering
Laboratory, Cincinnati, OH, to announce
key findings of the research project
that is  fully documented in a separate
report  of the same  title (see Project
Report ordering information at back).

Introduction
  The program is  one of  seven WRITE
programs nationwide in which EPA  and
cooperating states  or  local governments
evaluate and demonstrate the engineering
and economic feasibility of selected waste-
reducing technologies in a manufacturing
or fully  operational setting. The program
in Minnesota, which began in mid-1989,
targets the  metal finishing industry, spe-
cifically  rinsing processes within metal fin-
ishing operations.  The five technology
evaluations planned for the full life of the
Minnesota/EPA Program and subsequent
technology transfer activities are intended
to speed the early introduction of cleaner,
pollution-preventing technologies in  the
metal finishing industry.
  The report summarized here discusses
the  results of the first project performed
under the Minnesota/EPA WRITE program.
The project evaluated modifications  that
reduce drag out at a single plating line at
a printed circuit board  manufacturer.  It is
hoped that by demonstrating the success
of the modification in  a fully operational
setting, the technology will  be transferred
                                                                  Printed on Recycled Paper

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to other plating/rinsing systems within the
company as well as to other companies in
the metal finishing Industry.
  Two interrelated modifications that ef-
fectively help prevent wastes from entering
the rinsing processes are (1) reducing drag
out, which is the carryover of concentrated
solutions from  plating baths  and (2) re-
ducing rinse water flows. When drag out
is reduced, rinse water can be conserved
because less will  be needed to achieve
effective rinsing. EPA previously discussed
these changes to reduce  drag out and
rinse water use in the manual "Control
and Treatment Technology for the  Metal
Finishing  Industry -  In-Plant  Changes"
(EPA/625/8-82/008, 1982).

Procedure
  Mfcom, Incorporated, is a medium-sized, ,
job-shop circuit board manufacturer em-
ploying approximately 240 people  at its
plant in New Brighton, MN. Under a num-
ber of military and commercial  contracts,
the company produces an average of 1000
to  1200 ft2 of  double-sided  multilayered
panels per day. In 1989, annual revenue
was $17 million.
  The evaluation took place at  the sensi-
tize line where a number of process  baths
including etchant  (micro-etch),   activator,
accelerator, eloctroless copper, and rinse
tanks, first etch and then chemically de-
posit copper onto the  insides of the circuit
board through holes. Drag out from two of
the line's  process baths, the micro-etch
and the electroless copper, was a signifi-
cant source of waste copper discharged
into the rinse-water waste stream leaving
tha line. Figure 1  shows a schematic of
the micro-etch process,  and Figure 2 pro-
vides the same for the etectroless copper
process.   Rinse water from the two pro-
cesses had to be treated by an onsite, ion
exchange  unit for  copper removal before
it could be discharged to public sewer.
  Treatment of spent micro-etch, and
electroless baths included copper recovery
in both cases and regeneration  of etchant
in the case of the micro-etch solution.
When the micro-etch bath  had to be re-
moved from the  line and  replaced with
fresh bath, it  was company practice to
reclaim copper from  the bath as copper
sulfate and reuse it in another copper
plating solution onsite.  The etchant was
regenerated and also  used onsite for less
critical operations  such  as stripping cop-
per from carrier racks. The company also
recovered copper from the spent electro-
less copper bath, although the copper was
sent offsite for  reuse. Thus, copper-con-
taining bath solution retained in the process
baths after implementing drag out reduc-
tion changes would ultimately be subjected
to the company's recovery operations.
   To determine baseline drag out, samples
were taken at the process tanks and  at
the two rinse tanks following each process
tank — both before and after  a  rack  of
circuit  boards  was  moved  through the
three-tank system. Over a 2-week period,
12 sample sets were taken to calculate 12
baseline drag out values. Additional mea-
surements taken to  calculate drag out in-
cluded rinse-tank water volumes for each
of the  rinses; these volumes were  mea-
sured during each of the 12 sampling pe-
                                 riods. The total surface area of the boards
                                 plated for each rack was also tracked for
                                 each sampling period. Samples were ana-
                                 lyzed for total copper concentration.  The
                                 results of the copper analyses and the
                                 other data collected for  each sample set
                                 were used to calculate drag out with the
                                 following formula:
                                 Drag out:
                                 (ml/ft2)
                                         change in rinse copper
                                         concentration (mg/L)
                       rinse
                     volume (ml)
copper concentration in
process solution (mg/L)
board surface
  area (ft2)
                                                            Softened Water

             Micro-etch
             A
Counter
Current
Rinse
A
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Counter
Current
Rinse
A
A
Sampling
Location
                                           2.6 gpm
                                to treatment (Ion Exchange)
Figure 1. Micro-etch process diagram.
                                                             Softened Water
               Electroless
                 Copper
                A
                               Counter
                               Current
                                Rinse
                               A
  A
                                              3.3 gpm
   Sampling
   Location
                                 to treatment (Ion Exchange)

Figure 2.  Electroless copper process diagram.

                   2

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   To establish a baseline withdrawal rate
and drain times, both the withdrawal and
drain times were measured during each
sampling period.
   Two modifications to reduce drag out
were made and independently tested af-
ter taking  baseline samples. The  first
modification was to slow the  withdrawal
rate of the  racks as they were pulled from
the process tanks. The withdrawal rate of
a programmable mechanical hoist system
was slowed from the baseline  rate of 100
ft/min for the micro-etch line and 94 ft/min
for the electroless copper line to 11 ft/min
and 12 ft/min, respectively.  Samples were
taken  after the withdrawal  rates  were
slowed to  determine the effect  on drag
out.
   A second modification was then made
and tested: using  a withdrawal  rate be-
tween the  baseline and first modification
rates and increasing the drain time over
the  process tank  before transfer to the
rinse tank. The manually  operated  me-
chanical hoist had been taken out of ser-
vice because of persistent  problems with
break downs that predated  this study and
were unrelated to the evaluation; it  was
replaced with an air-assisted manually op-
erated hoist that the company also used
to operate the line. With the use of this
hoist, the second modification  withdrawal
rate was 40 ft/min for both the micro-etch
and the electroless copper baths. Drain
times were increased from  baseline drain
times of 3.4 sec for the  micro-etch bath
and 5.2 sec for the  electroless  bath  to
12.1  sec  and  11.9  sec,  respectively.
Samples were again  taken to determine
the effects of the intermediate  withdrawal
rate and longer drain times  on  drag out.

Results and Discussion
  The average drag out  for 12 sampling
sets of the baseline evaluation was cal-
culated at 12.1  ml  of bath solution per  ft2
of circuit board processed from the micro-
etch bath and 6.0  ml/ft2 from the  electro-
less copper bath. After the  first modifica-
tion, slowing the withdrawal rate,  the av-
erage drag out of  12 sampling sets was
calculated to be 6.7 ml/ft2 from the micro-
etch bath and 3.0 ml/ft2 from the  electro-
less copper bath.
  After the second modification, an inter-
mediate withdrawal rate and longer drain
time as compared with the baseline, the
average drag out of 12 sampling sets was
calculated to be 7.1 ml/ft2 from the micro-
etch bath and 2.9 ml/ft2 from the electro-
less copper bath.
  Results for the micro-etch  bath are sum-
marized in Table 1, and results  for the
electroless  copper bath are summarized
in Table 2. The reduction in drag out for
the micro-etch bath was 45% as a result
of the first  modification and 41 %  as a
result of the second  modification. For the
electroless bath, drag out was reduced by
50% after the first modification and 52%
after the second modification.
   For modification 1, the reduction in drag
out was calculated to prevent 194 g/day
of copper from the micro-etch bath and 9
g/day of copper from the electroless bath
from  entering the   rinse-water waste
stream. The figures for the second modifi-
cation were 180 and 9 g/day, respectively.
These figures assumed  a copper concen-
tration of 30 g/L in the  micro-etch bath;
2.4 g/L in the electroless bath; and a pro-
duction  level of 1200 ft2 of printed circuit
board per day.
   Economic calculations were based on
the cost of existing  treatment  and  dis-
posal methods for the rinse-water waste
streams. Onsite  ion-exchange canisters
with a capacity of 46  Ib copper treated the
rinse water.  When capacity was  reached,
canisters were regenerated offsite at $1096
per canister.  The economic  evaluation
showed  that the company could  save
$2640 per year in rinse water treatment
and disposal costs by implementing modi-
fication  1 or $2460  per year by imple-
menting modification  2. An additional sav-
Table 1. Summary of Micro-etch Results
                  ings of $710 per year for modification 1,
                  or $660 for modification 2, could be real-
                  ized in avoided water and sewer charges
                  if the company reduced  rinse-water flow
                  rates in proportion to the reduced copper
                  contamination resulting from the modifica-
                  tions.
                    No savings in process bath chemicals
                  could be calculated since the company's
                  chemical supplier based its charges for
                  chemicals on square feet of boards pro-
                  duced,  not on  the actual quantity  of
                  chemicals used.  Thus the company did
                  not receive economic incentive from the
                  chemical supplier to conserve  process
                  chemicals. If Micom could renegotiate the
                  cost of chemicals with the chemical sup-
                  plier based on reduced use, the econom-
                  ics  of the waste reduction modifications
                  would be improved. 	  -	   	

                  implementation
                    For a number of site-specific reasons,
                  the company decided to  implement a
                  longer drain time to reduce drag out in-
                  stead of altering the withdrawal rate. The
                  programmable mechanical hoist used for
                  modification 1 at Micom  was  unreliable,
                  often broke down, and was inflexible in its
                  programming. To slow the withdrawal rate
                  for modification 1, the vertical speed had

Baseline
Modification 1
Withdrawal Time of
Rate Withdrawal
(ft/min) (seconds)
100 1.7
11 14.9
Drain
Time
(seconds)
3.4
2.5
Total
Time
(seconds)
5.1
17.4
Drag Out
(ml/ft*)
12.1
6.7
slower rate of withdrawal

Modification 2
longer drain time with
intermediate withdrawal rate
 40
           4.3
                       12.1
                                    16.4
             7.1
Table 2. Summary of Electroless Copper Results


Baseline
Modification 1
Withdrawal
Rate
(ft/min)
94
12
Time of
Withdrawal
(seconds)
1.8
13.9
Drain
Time
(seconds)
5.2
3.2
Total
Time
(seconds)
7.0
17.1

Drag Out
(ml/ff)
6.0
3.0
slower rate of withdrawal

Modification 2
longer drain time with
intermediate withdrawal rate
40
           4.3
                       11.9
16.3
                                                2.9
                                                                                      •U.S. Government Printing Office: 1992— 648-080/60141

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to be adjusted. This adjustment slowed
not only the withdrawal rates for the micro-
etch and the electroless lines but also the
insertion rates. Further, these rates were
slowed for insertion and  withdrawal into
all tanks on the sensitize line, not just the
micro-etch and the electroless tanks. To
maintain production rates  at previous lev-
els,  operators supplemented  the  me-
chanical hoist with an air-assisted hoist.
  As a result of recurrent break  downs of
the mechanical hoist and the inability to
specifically target  and program slower
withdrawal rates for the two bath tanks,
the company took the mechanical hoist
out of service. Air-assisted hoists were
used as replacements. With this type op-
eration, it made more  sense for  the
company to implement a longer drain time
to achieve drag out reduction. The com-
pany believed  that it would be  easier to
train operators to increase the drain time
over the two  tanks than to  have them
stow withdrawal rates.
  For modification 2, the additional time
added to  the  sensitize line to  allow the
intermediate withdrawal rate  and longer
drain time, when compared  with  the
baseline, was 21  sec. This amount was
negligible when compared with the total
production time through the sensitize line
of 60 min. Minor modifications to the op-
eration of the line could offset the added
time so that the baseline  production rate
could be maintained. At Micom, filled racks
were often  held  beyond  the necessary
times in rinse tanks while being processed
in the sensitize line or were placed at the
loading area before entering the line.
Changes such as shortening the timing
between rack starts and/or reducing hold-
ing times in rinse tanks—times that were
known to be more than adequate — could
makeup for the added 21 sec.

Conclusions
  The waste reducing capabilities of two
simple, -drag-out-reducing  modifications
were successfully demonstrated at a Min-
neapolis area printed circuit board manu-
facturer. Economics were  favorable  for
both  modifications;  savings  were calcu-
lated at $3350 and $3120 per year for the
first and second modifications, respectively.
Since  no capital  costs were required to
make the changes, payback was immedi-
ate.
  Although both modifications looked fa-
vorable from the standpoints of econom-
ics and waste reduction capability, the first
modification, slowing the withdrawal rate
of the circuit boards from process  baths,
was  not  implemented by  the company
because of reliability and programmability
limitations of  the company's mechanical
hoist system. The company used the re-
sults from the second modification testing,
an intermediate withdrawal  rate  and a
longer drain time, in its decision to imple-
ment a longer drain  time for drag out
reduction.  The  implementation of this
change was dependent on training  opera-
tors to increase the drain time over tanks
and ensuring that this new operating pro-
cedure was maintained. The increase in
drain time did not slow production at the
company.
  The full report was submitted in fulfill-
ment of Cooperative Agreement No. CR-
815821-01-0 by the University of Minne-
sota, Minnesota Technical Assistance Pro-
gram (MnTAP) under the sponsorship of
the U.S. Environmental Protection Agency.
  The EPA author, Teresa M. Marten (also the EPA Project Officer, see below), is with the
      Risk Reduction Engineering Laboratory, Cincinnati, OH 45268, and Paul E. Pagel is
      with the Minnesota Technical Assistance Program, University of Minnesota, Minne-
      apolis, MN 55414-4504.
  The complete report, entitled "Modifications to Reduce Drag Out at a Printed Circuit
      Board Manufacturer," (Order No. PB92-198 555/AS; Cost: $17.00, subject to
      change) will be available only from:
          National Technical Information Service
          5285 Port Royal Road
          Springfield, VA 22161
          Telephone: 703-487-4650
  The EPA Project Officer can be contacted at:
          Risk Reduction Engineering Laboratory
          U.S. Environmental Protection Agency
          Cincinnati, OH 45268
United States
Environmental Protection Agency
Center for Environmental Research Information
Cincinnati, OH 45268

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