United States Environmental Protection Agency Air and Energy Engineering Research Laboratory Research Triangle Park, NC 27711 Research and Development EPA/600/SR-92/115 December 1992 EPA Project Summary Demonstration of Sorbent Injection Technology on a Wall- fired Utility Boiler (Edgewater LIMB Demonstration) P.S. Nolan, T.W. Becker, P.O. Rodemeyer, and E. J. Prodesky This document summarizes results of the full-scale demonstration of Lime- stone Injection Multistage Burner (LIMB) technology conducted on the coal-fired, 105 MWe, Unit 4 boiler at Ohio Edison's Edgewater Station. Developed as a technology aimed at moderate levels of sulfur dioxide (SO2) and nitrogen ox- ides (NOX) emissions control for rela- tively low-cost retrofit applications on older plants, LIMB operation at a cal- cium to sulfur (Ca/S) molar ratio of 2.0 is shown to be capable of achieving approximately 55 to 72% SO2 removal at capital costs significantly lower than wet flue gas desulfurization systems for units under 300 MWe and equal or lower operating costs. The removal depends upon the specific sorbent in use and the degree of flue gas humidification employed. Sorbents tested include a commercial calcitic hy- drated lime, both with and without a small amount of calcium lignosulfon- ate, a material added to improve reac- tivity. Results are presented for humidification of the flue gas both to an 11°C approach to the saturation tem- perature (where an increase of 10% [ab- solute] in SO2 removal efficiency is ob- tained), and for minimal humidification (where water is added solely to main- tain adequate electrostatic precipitator [ESP] performance). The performance of the DRB-XCL™ low-NO^ burners, with an overall average emission of 206 ng/ J (0.48 lb/106 Btu), is also presented. The document also discusses the im- pact of LIMB technology on boiler and plant operations. The effects are re- lated primarily to the increased quan- tity of particulate matter that must flow through the boiler, ESP, and ash han- dling equipment. The need for effec- tive sootblowing is seen as the single most important requirement when con- sidering application of the technology: without it, the increased particulate loading can decrease heat transfer effi- ciency between sootblowing cycles. The other effects discussed in some detail result from the quicklime compo- nent of the ash and the precautions that must be taken to avoid the poten- tial for deposits at wet/dry interfaces and for high pH conditions associated with ash handling. Finally, the application and econom- ics of the technology are discussed in terms of a hypothetical LIMB system on a 150 MWe boiler. This forms the basis for a comparison of the capital and operating costs of the technology with those of a conventional limestone wet scrubbing system. This Project Summary was developed by EPA's Air and Energy Engineering Research Laboratory, Research Tri- angle Park, NC, to announce key find- ings of the research project that is fully documented in a separate report of the same title (see Project Report ordering information at back). Introduction With the growing concern about acid rain and the improved understanding of its origins, an active program has been underway in the U.S. for many years to develop and utilize technology for acid Printed on Recycled Paper ------- rafn control. The focus of this effort has been on control of sulfur dioxide and ni- trogen oxides, (SO2 and NOX), from coal- fired utility boilers, since they represent the major source of these acid rain pre- cursors. National point source SO and NOX emission standards were established for utility boilers in the 1970s; however, these standards apply only to newly con- structed boilers. There exist today many coal-fired boilers built before establishment of these regulations. Many of these units have 20 to 30 years of remaining useful life, and the new acid rain legislation re- cently enacted by Congress will require some level of control for older units. The SOa emission standards for new boilers are based on the use of flue gas scrubbing technology, an option that may not be technically or economically fea- sible for existing boilers. Space for locat- ing the scrubber or disposing of its waste may not be available and/or the high capi- tal cost may not be justified for a boiler With a relatively short remaining lifetime. As a result, there is a need for low capital cost, easily retrofitted, control technolo- gies. The proposed acid rain legislation suggests that such technologies, which do not achieve the high removal efficien- cies of scrubbers, can still be important in meeting overall removal goals for existing boilers. One technology which could play a role in a utility's compliance with new acid rain legislation is LIMB (Limestone Injection Multistage Burners), which is based on the Injection of a dry sorbent into the boiler for direct capture of SO in the flue gas, combined with the use of low-NO burners for reduction of NOX emissions. l!lMB is a control technology for coal-fired boilers which requires low capital investment and is easily retrofitted to existing boilers. Al- though it achieves removal efficiencies lower than flue gas scrubbers, the cost per unit of SO., removed is much lower than that for scrubbers. Research and development work by the U.S. EPA and others in the late 1970s and early 1980s established the technical foundation for the design and operation of a LIMB sys- tem on a coal-fired boiler. In 1983 the LIMB process was consid- ered sufficiently developed to plan a full- scale demonstration of the technology on an operating utility boiler. EPA formally Initiated the demonstration in 1984 with matching co-funding by the Ohio Coal De- velopment Office. Babcock & Wilcox (B&W) was selected as the primary con- tractor and Ohio Edison's Edgewater Sta- tion in Lorain, Ohio, was selected as the host site; both of these organizations pro- vided funding support. The system was designed for Edgewater's 105 MWe Unit 4 boiler, a coal-fired unit burning a nomi- nal 3% sulfur Ohio coal. The LIMB system was started up in July 1987 after a thorough review of the research and development data base and subsequent design and installation. Initial operation showed that LIMB was highly effective in removing SO2, but that the system could be operated for only a few hours at a time due to the inability of the electrostatic precipitator (ESP) to control particulate emissions. This problem was diagnosed as being due to the inordinately high electrical resistivity of the LIMB ash. This situation made long-term, continuous operation impossible due to the need to maintain particulate emissions within the mandated opacity limit of 20% and 43 ng/ J. The Edgewater LIMB system was op- erated for several weeks intermittently in a series of 2 to 5 hour runs to gather SO2 removal data; then the system was shut down until the particulate removal prob- lem could be resolved. A maintenance shutdown of the Edgewater boiler had al- ready been scheduled at this time, so little project time was actually lost. At about this time B&W's dry scrubber experience and dry sorbent injection work by Consolidation Coal indicated that humidification of a flue gas stream in the presence of an active sorbent resulted in additional activation of the sorbent and enhanced SO removal from the gas stream. For LlMB, humidification offered the promise of increasing overall SO2 re- moval and sorbent utilization at a rela- tively small increase in cost. Flue gas humidification was also shown to solve the LIMB particulate problem, since mois- ture in the gas reduces the electrical re- sistivity of the ash, reduces the volume of the gas, and improves other electrical con- ditions. With the promise of increased SO2 removal beyond what was originally pro- jected and resolution of the ESP operat- ing problems, a developmental program was initiated to design and install a first- of-a-kind flue gas humidification system for Edgewater. A bypass arrangement was used at Edgewater due to the uncertain reliability of the humidifier at the time. Humidification in existing ductwork is envisioned for a commercial system, if site-specific limita- tions and design parameters permit suit- able residence time. The system started up again in Sep- tember 1988 and operated until June 1989 under a variety of test conditions, includ- ing some relatively long, steady-state, op- erating periods. The remaining portions of this document give results of the tests performed, and describe operating experi- ence with the Edgewater LIMB system. Results and Discussion of SO2, NOX, and Particulate Emission ' Control The original project goal for SO2 cap- ture, based on extensive bench and pilot scale tests, was 50% using sorbent at a calcium/sulfur (Ca/S) molar ratio of 2.0. During the initial test runs of LIMB in Sep- tember 1987, SO2 removal was approxi- mately 55 to 60% at a Ca/S of 2.0. With start-up of the humidifier in 1988, extended LIMB run times could be realized because of improved ESP operation, and the sys- tem could be adjusted and optimized. The humidifier added a potential complicating factor in the determination of LIMB SO removal, since SO could also be cap- tured in the humidifier itself. It was soon confirmed, however, that this removal oc- curred only at close approach to the adia- batic saturation temperature of the flue gas (about 52°C). Data taken while the humidifier was operated at high tempera- tures, typically about 135°C where ESP operation improved but no SO2 removal occurred, were used to determine SO removal in the furnace. Later tests with humidifier outlet gas temperatures ap- proaching the saturation point were used to define the incremental removal in the humidifier. However, unlike the 1987 tri- als when tests were limited to only a few hours, humidification stabilized ESP op- eration and thus permitted continuous op- eration and rigorous test periods with no significant changes in operating conditions extended to as long as 15 hours. The September 1987 tests included some runs using commercial, hydrated cal- citic lime treated with calcium lignosulfon- ate, an additive that appeared to improve SO2 removal in earlier bench scale stud- ies. Additional tests with more extensive use (1518 metric tons over two periods of 10 and 25 days each) of the modified sorbent were included in the 1988-89 dem- onstration. Tests were conducted with commercial hydrated calcitic lime both at "minimal humidification" and at an 11°C approach to saturation. The former term covers results obtained both before the humidifier was installed and when the hu- midifier was used just to maintain a suit- able flue gas temperature and humidity for effectiye electrostatic precipitation, nor- mally about 135°C. Corresponding tests were performed using lignosulfonate-doped sorbent. The data indicate that the modi- fied sorbent increases SO2 removal from 55 to 63% with minimal humidification, ------- and from 65 to 72% at close approach to saturation, when operating at a Ca/S of 2.0. The increase is believed to be due to a combination of the finer size and the nonagglomerating properties of the modi- fied sorbent, as well as the sorbent's abil- ity to resist sintering. SO2 Capture in the Furnace SO removal is determined by measur- ing SO at the stack and comparing this level with an uncontrolled calculated SO2 level based on the coal sulfur content. Typically the SO2 concentration falls rap- idly when sorbent is first injected into the boiler, and then continues to decrease gradually to a steady state value within about 30 minutes. This incremental in- crease in SO2 removal is thought to be due to supplemental reaction of sorbent that settles out on boiler surfaces. After this initial acclimation of the boiler, the SO2 levels remain relatively unaffected by sootblowing and other boiler operations since normally there is a continual re- newal of the deposits throughout such ac- tivities. Since pilot scale tests had indicated that SO2 removal was particularly depen- dent upon the temperature at the injection point, limited parametric optimization tests were conducted to quantify the effects at full scale. The variables, all of which are related to the temperature, included injec- tion at different elevations in the furnace, momentum flux ratio (essentially injection velocity and furnace penetration at a given load), the angle of injection (nozzle tilt), and boiler load. The results show that these parameters have little effect on SO2 removal in the Edgewater boiler over most of the ranges tested, indicating that the system is very insensitive to minor changes, if the initial design parameters enable near-optimum operation. The only factors that influenced SO2 removal significantly were those related to sorbent injection at the low end of the 1260 to 871 °C sulfation temperature win- dow or with a gross reduction in injection velocity. These conditions occurred when sorbent was injected at the upper eleva- tion in the furnace, and during periods when the boiler was at minimum load and/ or when the top row of burners were off. Under such conditions the estimated tem- perature at the injection point was 1038°C or lower and the increased residence time did not appear to be sufficient to compen- sate for the difference. At one point outside of the test period, the booster air was turned off entirely, leaving the lime transport air as the sole means of conveying the lime into the fur- nace. A dramatic loss in efficiency re- sulted, indicating that there is a point at which the momentum flux ratio becomes important. The condition was beyond the range of control on the booster air flow, however, and could not be readily tested. Injection into higher temperature zones was attempted in the form of tilting the injection nozzles at elevation 181 down 15° from horizontal. No appreciable change in SO2 capture was apparent. While this was not expected to lead to a dramatic difference, it leads one to sus- pect that elevation 181, where the tem- perature is about 1260°C, was very close to an optimum injection point for this boiler. Injection ports could have been located at a lower elevation where temperatures are higher; however, recirculation in the lower furnace would probably have resulted in sintering and decreased efficiency. SO2 Removal by Humidification The Edgewater project demonstrated that LIMB SO2 removal could be enhanced by humidification of the flue gas. Most of the tests conducted at close approach to the flue gas saturation temperature were limited to a period of 8 to 12 hours so that the baseline removal could be certified. The longest continuous run with no inter- ruption was 29 hours. Subsequently, how- ever, the humidifier has been operated continuously for as long as 11 days at an 11 to 14°C approach temperature as part of the Coolside process tests under the U.S. Department of Energy-sponsored LIMB Demonstration Project Extension. Humidification to an 11 °C approach tem- perature increases SO2 removal from 55 to 65% at a Ca/S of 2.0. The tests run at 22 and 33°C approach temperatures sug- gest that the enhancement is lost some- where slightly above a 33°C approach. However, the few data points obtained are not considered sufficient to define a truly representative curve. Pilot work and dry scrubber experience predict an expo- nential increase in SO2 removal when ap- proaching the saturation temperature. NOX Emission Control In order to reduce NOX emissions, the existing circular burners were replaced with B&W's DRB-XCL™ burners as part of the demonstration project. Discrete baseline tests with the older burners had shown emission levels of about 301 and 387 ng/ J at 63 and 97 kg/sec main steam flow (mid and peak load conditions, respec- tively). The DRB-XCL™ burners do not appear to be as sensitive to load condi- tions. An overall average NOX emission level of 206 ng/J was obtained over the full range of operating conditions during the January - June 1989 period. Aver- ages of the weighted 24-hour and 30-day rolling averages of 202 and 211 ng/J were calculated for the periods of January 8 to 26 and February 21 to April 22, 1989, respectively. The DRB-XCL™ burners operate at about 1.0 to 1.2 kPa pressure drop, in comparison to the 0.5 to 0.7 kPa required by the circular burners. The unburned carbon content averaged 1.54 wt % for four LIMB ash samples collected isokinetically while sorbent was being in- jected at a Ca/S of 2.0 and NOX emissions were about 206 ng/J. This would equate to about 4.6 wt % in an ash undiluted by reaction products and excess sorbent. It was also noted that there appeared to be no interactive effects between sorbent in- jection and NOX reduction. Particulate Emission Control An early concern of the LIMB demon- stration was the ability of the Edgewater ESP to handle the two- to threefold in- crease in particulate loading that accom- panied sorbent injection. While the load- ing and the finer size of the particulate are issues that must be addressed, the pre- liminary tests in 1987 dramatically indi- cated that the extremely high electrical resistivity of unconditioned LIMB ash was by far the most immediate impediment to continuous operation. As noted earlier, the high resistivity, in particular, precluded continuous operation beyond several hours as the opacity climbed toward the 20% limit at that time. Fortunately, the humidi- fier installed for the 1988-89 operations proved to be an effective means of condi- tioning the ash and restoring the efficiency of the ESP to near normal levels. Although the Edgewater humidifier was designed to accommodate close approach to saturation for SO2 removal purposes, it was soon found that adding even modest amounts of water (lowering the flue gas temperature to about 135°C) was suffi- cient to maintain opacity generally in the 1 to 7% range throughout the demonstra- tion. Specific ESP tests included mea- surement of resistivity in situ, operating voltage and current, and inlet and outlet gas flow, mass loading, and particle size distribution. These intensive tests were conducted during the week of May 22, 1989, and cover operation of the ESP with both three and five of the six fields in service while the unit was operating at 75 MWe, due to operational concerns be- yond the control of the project. Neverthe- less, the conditions were such that the humidifier was operating at the full design ------- flow since repairs to various sources of air In-leakage in the boiler had not been fully successful. For the tests, the ESP inlet temperature was maintained at 135°C except for one test with an inlet temperature of 74°C. The results of these tests, coupled with those from associated laboratory tests and mathematical modelling, indicate that humidiflcation to 135°C lowered resistivity to 2.3 x 10" ohm-cm, permitted continu- ous operation at acceptable opacity lev- els, and resulted in paniculate emissions on the order of 1.7 to 8.6 ng/J or less at the conditions tested. LIMB Commercial Design and Economics Two LIMB retrofit systems were de- signed for a 150 MWe boiler to allow comparison of the costs and impacts with those of a wet flue gas desulfurization (FGD) system. Previous economic stud- ies had shown LIMB to have cost advan- tages over wet FGD for units under 300 MWe, while wet FGD was more cost ef- fective for larger units. A representative unit firing 2% sulfur coal was used as a basis. Complete costs of the two LIMB system designs were estimated, and the resultant operational changes analyzed. The two systems were selected to cover the range between the high cost when humidification to an 11°C approach tem- perature is used to obtain maximum sulfur capture and the lower cost system where minimal humidification only restores ESP performance. The main difference be- tween the systems is the inclusion of a humidification chamber for the maximum humidification case, while the minimal humidification design included installation of humidifier lances in existing flues. Results of the analysis show that LIMB system capital costs are in the range of 30 to 43% of a wet FGD system, and that the costs per ton of SO2 removed are lower than those of equivalent performance Wet FGD systems. Additionally, the ad- vantages of the LIMB systems include: simplicity of operation and ease of main- tenance, reduced outage time for installa- tion, shorter lead time for material supply, smaller space requirement, and lower re- duction of plant electrical output Operational Considerations LIMB Effects on Boiler Operation The impact of LIMB technology on boiler operation is related primarily to increased particulate loading and depends heavily on the adequacy of the sootblowing sys- tem. With sorbent injection in the upper furnace as was done at Edgewater, LIMB technology results in a higher rate of ash accumulation on tubes and other avail- able surfaces, roughly in proportion to the additional particulate matter. Virtually all of the sorbent appeared to follow the gas stream through the convective pass, rather than being reported as bottom ash. Thus injection at the elevation of the nose and above avoids the potential for sintering and slagging conditions that would prob- ably have resulted had the sorbent been introduced at a higher temperature and/or a lower elevation. The four new steam sootblowers added in the primary super- heat area as part of the project were ef- fective within their range, but did not make up for limitations elsewhere. The LIMB ash that did accumulate on the tubes was found to be about as easily dislodged by sootblowing as is normal coal fly ash. The most notable difference was that, instead of operating on a normal once-per-shift basis, the sootblowers were run about three times as frequently, effec- tively in almost continuous cycles. As one might expect, this strained the capac- ity of the compressed air system at Edgewater, to the point that all but the four air heater blowers were converted to a steam-driven system for the LIMB ex- tension work to follow. This is not to say that an air system would not work, only that the capacity of the Edgewater system could not keep up with the heavier duty cycle. The overall effect of ash accumulation on the tubes was a decrease in heat trans- fer and higher flue gas temperatures throughout the boiler. Heat transfer rates through the tubes appeared to return to normal immediately after being blown, only to begin the cycle once more. Because of this and the relatively low capacity of the air-driven sootblowers, the net result was a flue gas temperature of about 177°C at the air heater outlet, compared to a more normal temperature of about 149°C under steady state conditions. However, effec- tive sootblowing is expected to -reduce this temperature rise significantly. The other source of energy loss neces- sarily associated with LIMB is the excess air used both for sorbent dispersion in the furnace and water atomization in the hu- midifier. At Edgewater, ambient air was used for both, although preheated air, recirculated flue gas, or even mechani- cally assisted devices could be used for sorbent dispersion in another installation. While the data have not been reduced in terms of a specific energy loss, the "booster air fan" arrangement at Edgewater used about 3.78 kg/sec of air to feed 1.51 kg/sec of sorbent into 126 kg/sec of flue gas. Humidification to an 11°C approach to saturation required about 2.52kg/sec of air to atomize 5.54kg/sec of water. The atomization system was designed conser- vatively with an air compressor motor rated at 876 kW, to ensure the production of the fine droplet size required. Close approach to saturation at Edgewater also required flue gas reheat for plume buoyancy. A steam coil reheater with the capability of raising the flue gas temperature 22°C was installed for this purpose at the outlet of the ESP, just before the induced draft fan. In applications where only minimal humidification would be required for ESP operation, the energy penalty associated with high levels of humidification and re- heat would be significantly lower. Humidifier Operation The humidification system installed at Edgewater proved to be relatively prob- lem-free and achieved the purposes for which it was designed. Early mathemati- cal and plastic flow modelling and quarter- scale simulation tests, all conducted in the early design phase, provided mean- ingful insight into the flow patterns and evaporation processes involved. For the most part, the wet/dry interface problems were limited to relatively small, manage- able areas. The most significant problem was a buildup of material near some of the atomizers. The material would build to several centimeters in length and then fall to the floor of the horizontally config- ured chamber where material would accu- mulate. A modified airfoil lance assembly for the atomizer array was designed and installed in 3 of the 22 lance locations for the last 3 months of the program. These modified assemblies had a greatly reduced tendency for deposit formation, and the complete atomizer array was replaced be- fore continuing with the Coolside process tests. When the humidifier was operated at outlet temperatures 22°C and above the saturation temperature, essentially no dif- ficulties were encountered. Moreover, the presence of unreacted quicklime, CaO, in the ash undoubtedly contributed to favor- able conditions by virtue of its exothermic reaction with water. Although the quantity of water vapor present in the flue gas as a result of combustion was more than suffi- cient for total rehydration of the CaO, the gas/solid reaction kinetics appeared to be quite slow when the humidifier was oper- ated considerably above the saturation temperature. Under this operating condi- ------- tion, much steam evolved when mixing LIMB ash with liquid water just prior to disposal (described in more detail later). Notably less steaming occurred when the humidifier was operated at close approach to saturation, suggesting that, whatever the mechanism(s), the excess CaO has a strong affinity for liquid water. Predictably, deposits formed in the cen- ter area of the humidifier outlet turning vanes after extended operation precisely at an 11°C approach to saturation. The deposits built to a thickness of about 10cm and then sloughed off onto the floor. These deposits are not considered to be a problem because the chamber was be- ing tested at the extreme limit of its de- sign and several remedial alternatives could be used in a commercial system. These include not only operation at a slightly higher temperature, but also inten- tional capture of large, unevaporated drop- lets with periodic deposit collection and removal through a hopper system. If site- specific spatial limitations permit, a verti- cal, down-flow configuration with a hopper for solids collection would be preferred for a commercial humidifier required to oper- ate at close approach temperatures. Ash Handling and Disposal LIMB technology also has significant im- pacts on the power plant's ash handling and disposal practices. The most obvious of these is the sheer quantity of material that must be processed. As implied ear- lier, operation at a Ca/S of 2.0 with a 10% ash, high sulfur coal almost triples the rate at which ash must be collected by the ESP and then transferred to the ash silo. As long as lines were free of obstructions and the transfer equipment was in good working order, the increased quantity gen- erally did not pose a problem since nor- mal demand and the basic design of the ash handling system could accommodate such amounts. By the same token, it was important to react to upsets quickly since there was less time available to make required repairs. Beyond the quantity of ash itself, the other major considerations regarding LIMB ash handling and disposal stemmed from the quicklime component and the pozzo- lanic properties of the ash. At Edgewater, ash is pneumatically conveyed from the ESP hoppers into the ash storage silo. Even during the relatively short tests in 1987, LIMB ash tended to bridge over at the wet/dry interface near the aspirating water jets used to create the vacuum. A device designed to ram through the de- posit periodically was successfully de- signed and installed to overcome this seemingly small, but critical, problem. Greater difficulty was encountered due to the amount of steam generated by the water/quicklime reaction occurring in the beds of the trucks used to haul ash to the landfill. Water was mixed with dry LIMB ash from the silo in a pug mill that dis- charged directly into the truck waiting be- low. As the level rose in the bed, the steam that resulted soon made it impos- sible for the operator to see how much room remained. As noted earlier, this was true especially when minimal humidification was employed. Although the problem had been anticipated and a large fan had been mounted to blow or suck the steam away, the severity of the steaming was far beyond the fan's capa- bility. After considering a number of alter- natives including weighing and sonic tech- niques, a system was devised that in- volved the operator's lowering a freely hanging thermocouple to the desired fill level in the empty truck bed. The thermo- couple then read ambient temperature up until the time it would begin to sense the hot ash. While not regarded as a perma- nent "commercial" solution to the problem, it proved to be an expedient, practical remedy for the purposes of the demon- stration. In time, a "reference" thermo- couple was added in the discharge chute of the pug mill, since some variation in temperature did occur, typically in the 66 to 121°C range, depending on the stoichi- ometry and degree of humidification. For future commercial systems, a more sophisticated design including those based on gravimetric, sonic, or even spectropho- tometric techniques is envisioned, if treat- ment is restricted to an ash unloading system such as exists at Edgewater. As- suming that rehydration of the quicklime component is the preferred method of ash disposal, another extreme is possible where there are pre-existing facilities, such as a pug mill and radial stacker at the disposal site, which can readily accommo- date steam from the ash. The steam emanating from the surface of the ash presents no sustained problem in that it subsides to faint wisps within about 15 minutes. Before the steaming problems were brought under control, they gave rise to a further complication that had been under- estimated. While underfilling the truck was the norm, on a couple of occasions overfills did occur that had to be picked up with a front end loader. The area then was washed down as a final cleanup mea- sure. When this was done, the lime-rich ash would raise the pH of water draining toward the plant's ash pond. While provi- sion had been made for sensing and neu- tralizing high pH water that could result from a failure in the pneumatic ash con- veying system and from minor yard spills of lime or ash, the amount that spilled from overfilling the truck had not been anticipated. Moreover, sumps that accu- mulate significant quantities of lime or LIMB ash due to low flow or agitator failure could also produce undesirably high pH. The solution to all of these related difficul- ties was rerouting all of the potential sources through the neutralization system. Most of the LIMB ash from Edgewater was placed in Ohio Edison's ash disposal site, adjacent to the normal ash disposal area. Despite apprehensions that the cementitlous properties of the ash might cause some difficulty with the bulldozers, no significant problems were encountered, probably because the pozzolanic reactions did not proceed to any appreciable extent at the relatively low water/ash ratios used to produce a material that can be readily dumped from the truck. In addition to the routine LIMB ash disposal, approximately 140 truckloads were placed in two test cells in an isolated area of the disposal site for study over the next several years under a related DOE-sponsored program. Summary and Conclusions The results of the LIMB demonstration project on a full-scale, coal-fired utility boiler show that the technology has met or surpassed program goals with respect to SOg and NO emission control. More- over, in spite of early difficulty in control- ling particulate emissions with the ESP, the design and installation of a full-scale humidification system appears to have overcome the adverse aspects of the in- creased quantity of fine, high resistivity ash. Specifically, the use of a lignosulfon- ate-doped hydrated calcitic lime, produced in bulk by a commercial supplier, and op- eration of the humidifier at an 11°C ap- proach to saturation resulted in SO re- moval efficiencies of up to 72% at a Ca/S of 2.0, far in excess of the 50% program goal. Even without the lignosulfonate ad- ditive, up to 65% capture was possible under the same conditions. Removal effi- ciencies of about 62 and 55% were ob- tained in the absence of humidification to the close approach temperature for the modified and unmodified sorbents, respec- tively. The SO2 data have also been reduced and presented in a form that char- acterizes the removal over a range of stoichiometric ratios. At the same time, an overall average NOx emission level of 206 ng/J was achieved over months of operation with the DRB-XCL™ burners in- stalled to meet a goal of 215 ng/Jor less. Particulate emission control was effectively restored by modest levels of humidification ------- as indicated by opacity measurements at the ESP outlet. Particulate mass emis- sion levels of 4.3 to 8.6ng/J were found to be far below the 43ng/J goal, although the tests had to be conducted at condi- tions representing approximately 75% of the full boiler load. This load limitation was imposed because long-term loss of refractory material had exposed support beams in the vicint'ry of the nose arch to unaccepatably high temperatures. The designs of two 150 MWe LIMB systems, one with only minimal humidification to restore ESP efficiency and another with the capability of operat- ing at close approach to saturation, were used as a basis for cost comparisons with wet limestone FGD. Economic studies have shown that the capital and operating costs of LIMB technology compete favor- ably for units up to about 300 MWe. Ad- ditional benefits of LIMB include ease of operation and maintenance, relatively simple installation, smaller space require- ment, and a lower reduction of the plant's generation capacity. The overall impact LIMB technology had on boiler and plant operations at Edgewater is particularly notable in a few areas, all of which are considered man- ageable when viewed from the perspec- tive of further commercialization. The single greatest impact comes simply from in- creased particulate loading through the boiler, ESP, and ash handling system. Unless restored by effective sootblowing, heat transfer efficiency in the boiler de- creases in proportion to the amount of sorbent injected. At higher Ca/S ratios the limitations of the compressed air sootblowing system at Edgewater soon pointed toward the need for future com- mercial systems to address sootblowing capability more thoroughly than had origi- nally been anticipated for the demonstra- tion project. In comparison with these effects, the impact of increased gas flow from air used to disperse the sorbent and to atomize water in the humidifier is thought to be quite low, especially if only moder- ate humidification to perhaps 135°C is re- quired to restore ESP efficiency. While the data indicate an overall energy pen- alty of about 1.5% in boiler efficiency for the combined impacts, it is strongly be- lieved that this can be recovered with more effective sootblowing. Again because of the increased quan- tity of material, LIMB technology makes additional demands upon the ash han- dling system that must be taken into ac- count in the application for future com- mercial systems. Beyond this, the chemi- cal composition of the LIMB ash, and the quicklime component in particular, should be reviewed carefully in light of possible deposit formation at wet/dry interfaces where the pozzolanic properties of the ash can be important. Likewise the lime component of the ash is important with regard to potentially high pH conditions in any wetting operation that might be used as part of the ash disposal process. •U,S. Government Printing Office: 1993 — 750-071/60164 ------- ------- P. Nolan, T. Becker, P. Rodemeyer, andE. Prodeskyare with the Babcock& Wilcox Co., Barbeton, OH 44203. David G. Lachapelle is the EPA Project Officer (see below). The complete report, entitled "Demostration ofSorbent Injection Technology on a Wall-fired Utility Boiler (Edgewater LIMB Demonstration)," (Order No. PB92-201 136/AS; Cost: $35.00, subject to change) will be available only from: National Technical Information Service 5285 Port Royal Road Springfield, VA 22161 Telephone: 703-487-4650 The EPA Project Officer can be contacted at: Air and Energy Engineering Research Laboratory U.S. Environmental Protection Agency Research Triangle Park, NC 27711 United States Environmental Protection Agency Center for Environmental Research Information Cincinnati, OH 45268 Official Business Penalty for Private Use $300 BULK RATE POSTAGE & FEES PAID EPA PERMIT No. G-35 EPA/600/SR-92/115 ------- |