United States Environmental Protection Agency Risk Reduction Engineering Laboratory Cincinnati, OH 45268 Research and Development EPA/600/SR-93/144 September 1993 Project Summary Evaluation of Ultrafiltration to Recover Aqueous Iron Phosphating/Degreasing Bath Gary D. Miller, Timothy C. Lindsey, Alisa G. Ocker, and Michelle C. Miller Pollution prevention efforts studied in the report summarized here targeted the hazardous waste generated from a 5000- gal iron phosphating/degreasing bath used by a metal fabricator to clean and precon- dition steel parts for painting. When oil buildup in the bath began to sacrifice prod- uct quality and the discharge levels of oil and grease in the rinse water edged closer to the maximum allowable limit, all 5000 gal were dumped and replaced. Periodic dumping, about three times each year, resulted in at least 15,000 gal/yr of hazard- ous waste. Several waste minimization al- ternatives were considered, and ultrafiltra- tion was selected as the most promising technology to recover and reuse the bath and to reduce the total amount of hazard- ous waste generated. This project was carried out in four stages: (1) initial assessment of the prob- lem and evaluation of alternatives, (2) bench-scale screening of Ultrafiltration membrane candidates, (3) pilot-scale study at the Illinois Hazardous Waste Research and Information Center (HWRIC), and (4) full-scale implementation and testing onsite at the company's facility. Full-scale testing integrated the new waste reduc- tion scheme into the facility's production process by applying Ultrafiltration directly to the 5000-gal iron phosphating/ degreasing bath. Ultrafiltration success- fully removed oil contamination from the bath and returned clean process solution back to the original 5000-gal tank. Ultrafil- tration concentrated the hazardous com- ponent down to 10 gal of oily waste and reduced hazardous waste generation 99.8%. Permeate flux rates were high enough to compete with the constant in- put of oil from the production line, and concentrations of oil in the bath were main- tained at acceptable operating levels. The estimated payback period associated with implementing Ultrafiltration was only 6.9 mo. This Project Summary was developed by EPA's Risk Reduction Engineering Laboratory, Cincinnati, OH, to announce key findings of the research project that is fully documented in a separate report of the same title (see Project Report order- ing information at back). Introduction The objective of the U.S. Environmental Protection Agency (EPA) and the Illinois HWRIC was to evaluate potential technolo- gies and operational modifications that could reduce the amount of hazardous waste gen- erated at a metal fabrication facility. The goal of this project was to find an environmentally responsible means to extend the life a 5000- gal iron phosphating/degreasing bath and thereby reduce hazardous waste generation. The relative feasibility of Ultrafiltration as well as its capability to reduce waste generation were assessed on an engineering and eco- nomic basis. Results of this project were used to justify installing a permanent Ultrafiltration system and operating practices that would improve product quality. Industrial Participant R.B. White, Inc., of Bloomington, IL, oper- ates a sheet metal fabrication facility that manufactures painted steel shelving units. Cold-rolled steel arrives at the plant from the steel mill coated with mill oils to protect the ^Ci Printed on Recycled Paper ------- bare metal from corroding or staining during storage and fabrication operations. During fab- rication, coolants and lubricants are also ap- plied to the metal working surface. Before being painted, the metal surfaces are cleaned to remove the mill oils and metal working fluids and then preconditioned to bond well with the paint coating. Fabricated parts are cleaned and phosphated in a 5000-gal heated, aqueous immersion tank and rinsed with a fresh water spray. The company previously operated separate degreasing and phosphating tanks using trichbroethylene in the degreasing tank and in 1985, switched to a single-stage aqueous iron phosphating/ degreasing system to improve worker safety and reduce the generation of organic solvent emissions and hazardous waste. Although the switch eliminated the risks and liabilities associated with organic solvents, it introduced a new waste disposal problem. Problem Description Simultaneous degreasing and phosphating in the same bath formed an oil-water emul- sion. With extended use, the buildup of oil in the bath reduced cleaning and phosphating efficiency, and product quality was compro- mised. Additionally, dragout of oil from the bath into the rinse water eventually pushed oil and grease levels in the discharge over the allowable limit. In the past, oil skimmers were used to control oil slicks on the surface and prolong the life of the bath, but the skim- mers were only partially effective. When oil in the bath began to sacrifice product quality and the discharge levels edged closer to the maximum allowable limit, the bath had to be replaced. Depending on production rates, the bath typically lasted 3 to 4 mo. Replacing the bath required a full day of lost production time to take the process off-line, make arrange- ments with a waste transporter to drain and dispose of the entire contents, and recharge the tank with 5000 gal of fresh water and raw materials. The spent bath was classified as RCRA hazardous waste because it failed Toxicrty Characteristic Leaching Procedure (TCLP) tests for xylene. Since land disposal of liquid wastes is prohibited, the bath, sludge, and skimmed oil were incinerated in a ce- ment kiln. Disposal costs including transpor- tation and incineration ran about $1/gal which came to $5000/bath, or about $15,000/yr in addition to the costs associated with lost pro- duction time and replacement of water and raw materials. Process Background Iron phosphating/degreasing processes are widely used in the manufacture of metal prod- ucts to clean and precondition ferrous sur- faces. Many metal fabricators and others that paint or coat steel choose iron phosphating/ degreasing processes because they effec- tively clean metal parts, provide an excellent surface for paint adhesion, and protect against under-paint corrosion. The goals and mecha- nisms associated with the degreasing and phosphating process are discussed bebw. The goal of degreasing is to remove mill oils, metal working fluids, and any other shop soils from the steel surface and prepare it for finishing. Degreasing was accomplished us- ing nonbnic surfactants in a heated (140°F), air-agitated bath. The surfactants surrounded the oil and dirt particles and formed a stable emulsbn that cleaned the parts and pre- vented the oil and dirt from redepositing on the metal surface. Phosphating is a common type of pre- paint coating process used to simultaneously provide corrosion resistance and enhance paint adhesion to a metal surface. Phosphate salts chemically bond to the metal surface to produce an amorphous conversbn coating. The phosphate conversbn coating is non- conductive so it protects the metal surface from electrochemical oxidation that leads to rust and corrosbn. The matrix of the phos- phate coating forms capillaries that increase the surface area and provide a mechanical interlocking structure on which the paint can adhere. The 5000-gal bath was charged with Dura- Gard Soke and Tart liquid acid (supplied by DuBois Chemicals),* which contained non- ionic surfactants, phosphate salts, phosphorb acid, and accelerators to promote phosphate precipitation. The concentratbn of Dura-Gard Soke and the pH in the bath were checked daily with a simple titration kit and litmus paper to ensure that concentrations were maintained between 1.5 and 2.0 oz Dura- Gard/gal and at a pH of 3.5. Waste Reduction in the Metal Fabricated Products Industry The EPA's campaign for waste reduction is bringing change to industries through the 1984 Hazardous and Solid Waste Amend- ments (HSWA) to RCRA, the Toxics Release Inventory (TRI), the 1990 Pollution Preven- tion Act (PPA), and the more recent 33/50 Program. The HSWA require industries to set up waste minimization programs and to pro- duce certified manifests demonstrating their waste reduction efforts. The TRI is a comput- erized data base that tracks the routine and accidental release of approximately 300 toxic chemicals reported by U.S. manufacturers. The 1990 PPA brought about stricter TRI industrial report requirements that include pro- viding information on pollution prevention ef- forts. The 33/50 Program is EPA's voluntary "Mention of trade names or commercial products does not constitute endorsement or recommendation for use pollution preventbn initiative to reduce the Natbn's releases of 17 TRI chemicals 33% by the end of 1992 and 50% by the end of 1995. Backed by federal legislatbn and eco- nomic incentives, EPA's pollutbn preventbn campaign has targeted several operatbns associated with the metal fabricated products industry. Finding environmentally responsible solutions to the industry's waste disposal prob- lems has focused on source reductbn (in- cluding process modifications and raw mate- rials substitution) and recycling. The EPA recommends various strategies for pollution prevention in the metal fabricated products industries. Until now, waste reduc- tion in surface preparation operations has focused on conserving or finding alternatives to organic solvent cleaners. For years, the metal finishing industry has relied on organic solvents for cleaning metal parts. Trichbroet- hylene, methylene chloride, perchloroethyl- ene, and 1,1,1-trichloroethane account for a majority of the chbrinated solvents used by industry. Recently, however, environmental concerns for health and disposal conse- quences have increased. Chbrinated solvents were not only targeted by the TRI and 33/50 Program, but solvent wastes were among the first to be banned from land disposal by the 1984 HSWA. More recently, 1,1,1- trichloroethane has been linked to ozone depletion in the upper atmosphere and will no longer be manufactured in the U.S. after 1995. As restrictbns increased the cradle-to-grave liability for solvent waste generators, the metal finishing industry began to turn to other op- tions for cleaning operations. Aqueous clean- ers, emulsion cleaners, mechanical and ther- mal methods, and abrasive cleaners emerged as alternatives to organb solvents. These optbns help reduce emissions of volatile or- ganb compounds (VOCs) and lessen worker exposure. The switch to aqueous cleaners can also reduce the annual reporting required under SARA Title III, Section 313, Toxic Chemical Release Reporting: Community Right-To-Know. Aqueous cleaners have already replaced solvent degreasers in many industrial surface preparation operations. The water-based cleaners effectively remove protective oils, cutting oils, hydraulic fluids, silbone oils, wa- ter soluble coolants, shop dirts, finger prints, and other soils. Special additives also make the aqueous cleaners versatile coating solu- tbns. Making the switch has even made it possible to eliminate some separate degreasing and coating processes as well as reduce waste generation. Aqueous cleaners are finding success in many industrial surface preparation operatbns including airplane com- ponents, printed circuit boards, advanced com- posites, fasteners, and automotive parts. The tank life of the aqueous cleaners is limited by the buildup of the dirts and oils in ------- the bath. Cleaning effectiveness begins to deteriorate, and the performance of other chemicals in the bath is inhibited. Although the aqueous degreasers do not carry all the risks and liabilities associated with the dis- posal of waste organic solvent cleaners, peri- odic replacement of the bath creates a differ- ent waste disposal problem. Current disposal options for spent aqueous cleaning solutions include tankering, incinera- tion, or discharge. The rising costs associ- ated with these disposal and pollution control options are the main incentives to extend the life of the aqueous cleaner baths. Rather than wasting valuable raw materials, the aqueous cleaners have the potential to be recycled again and again. Depending on the physical characteristics of the bath solution, the life of the bath can be extended by skimming con- taminants off the top, settling heavier frac- tions to the bottom, or filtering out suspended species. Ultrafiltration Conventional filtration techniques rely on depth or screen filters to remove oil and dirt from a process solution, but conventional fil- ter media clog easily. They require frequent backflushing or disposal, which result in addi- tional wastes. Membrane filtration is a more advanced technique that takes advantage of thin-film membranes and turbulent flow pat- terns to deliver a more consistent flow rate and a higher quality filtrate than conventional filtration. Ultrafiltration is one class of mem- brane filtration that uses membranes with pore diameters ranging from 10'9 to 1Q-6 m. The Ultrafiltration process works by produc- ing two separate streams: concentrate and permeate. The permeate stream contains only the components in the feed solution small enough to pass through the membrane pores (water, solubilized species). The con- centrate stream contains everything else that is rejected by the membrane (emulsified oil and dirt). The recent development of more durable membranes, such as PVDF, has expanded the application of Ultrafiltration beyond its ori- gins in the food industry to successfully handle industrial process solutions with extreme pHs, high temperatures, and high oil concentra- tions. Because of its unique capabilities to concentrate oily wastewater and produce a clear filtrate, Ultrafiltration has emerged as a promising technology for extending the life of aqueous cleaner baths. Ultrafiltration of oil- water emulsions is a more straightforward method for removing and concentrating oil than are other physical, chemical, or thermal means. Ultrafiltration does not require a stock- pile of chemicals and does not produce a chemical sludge that requires special treat- ment or disposal. Instead, Ultrafiltration pro- duces a water phase that requires no further treatment and a concentrated phase only a fraction of the original volume that can sus- tain combustion or be disposed of efficiently. Ultrafiltration requires no heat input, low en- ergy, and little operator attention. One of the greatest limitations of Ultrafiltra- tion membranes is their tendency to foul. Fouling is detected as the decrease in per- meate flux over time, where the flux is de- fined as the volumetric flow rate of permeate per cross-sectional area per time. Fouling is mainly due to the accumulation of particles on the membrane surface and/or within the pores of the membrane itself. In industrial applications where Ultrafiltration could be used to filter aqueous cleaning baths, fouling will typically be due to oils, suspended solids, free surfactants, and metal precipitates. When a membrane shows signs of fouling, the flux can largely be restored by cleaning the mem- brane, but a portion of the flux may be unre- coverable because of irreversible fouling. Full-Scale Testing Results from the bench- and pilot-scale studies were used to develop a full-scale, modified-batch test conducted onsite at the facility. Figure 1 shows how the full-scale test applied Ultrafiltration directly to the 5000-gal iron phosphating/degreasing bath. The objec- tive was to directly measure the effect of Ultrafiltration on the process solution under actual plant conditions. The full-scale test took into account the constant input of oil from the production line and the daily addition of bath chemicals. Additionally, the full-scale test also helped identify problems with the Ultrafiltration equipment and anticipate changes that should be made on a permanent unit. The full-scale in-plant testing featured an Ultrafiltration system provided by Koch Mem- brane Systems (Model UF-4) equipped with four 1-in tubular PVDF membranes (100,000 Concentrate Pump ffrr Men brane Permeate to bath Figure 1. Modified-batch scheme Ultrafiltration. MWCO, 4.4 sq ft total area). Data obtained from the full-scale modified-batch test was used to determine whether Ultrafiltration would be a viable option for waste reduction at the plant. Technical, operational, and economic aspects associated with the Ultrafiltration equip- ment were examined to evaluate the feasibil- ity of this technology to improve the company's metal fabrication operation. When field testing began, the iron phosphating/degreasing bath had not been replaced in over 3 mo. The aqueous solution was murky with dirt and oil, and large patches of free oil floated on the surface. The changes that took place over the next 11 days of Ultrafiltration testing produced a dramatic ef- fect. Surface oil slicks disappeared and were replaced by a clean, light foam. The bath solution was visibly clearer, and plant person- nel testified that it looked like a freshly re- charged bath. Results of total organic carbon (TOC) analyses for the full-scale testing showed the change in oil and surfactant con- centrations during the test (Figure 2). Economic Analysis The costs and benefits associated with installing an Ultrafiltration system were ana- lyzed to determine the economic feasibility of this technology. Based on the estimated ex- penditures and savings, the payback period associated with this technology, was only 6.9 mo. The net present value and interest rate of return indices were $152,143 and 178%, re- spectively. Therefore, investment in an ultra- filtration system represented a very attractive economic alternative. Conclusions The overall evaluation of this pollution pre- vention project was based on Ultrafiltration performance, product quality, and econom- ics. Results indicated that the concentration of oil in the iron phosphating/degreasing bath was substantially reduced and maintained at acceptable operating levels. Virtually all of the unused phosphating agents were conserved although a portion of the unused surfactants was not. Permeate rates exhibited excellent performance during the acidic (pH=3.5), high temperature (140°F) operation and were high enough to process the constant input of oil from the production line. The entire 5000-gal bath was processed in 180 Ultrafiltration oper- ating hours. Coating weight, rust creepage, and paint adhesion tests conducted by DuBois Research Laboratory and plant personnel on samples of steel parts indicated that product quality achieved during the full-scale study was good for the plant's application. The payback period for implementing the Ultrafil- tration system was 6.9 mo. By using Ultrafil- tration, the company will reduce its hazard- ous waste generation by at least 15,000 gal/ yr, a 99.8% reduction. £l).S. GOVERNMENT PRINTING OFFICE: 1993 - 7«NMm/moS9 ------- 300 , 200 -1 O roo Increased surfactant due to increased Dura-Gard additions 'Surfactant Oil 0 100 200 Operating Time (hours) Figure 2. Oil and surfactant in bath vs time. This project has successfully demonstrated the ability of membrane filtration to reduce hazardous waste generation and recover valu- able raw materials in a metal fabrication op- eration. This application introduces another innovative waste reduction technique to the metal fabricated products industry that could benefit the many plants nationwide that use aqueous cleaner systems like the iron phosphating/degreasing process at the R.B. White company. The ultrafiltration system implemented in this project saves money, maintains good product quality, and reduces waste generation. G.D. Miller, T.C. Lindsey, A.G. Ocker, and M.C. Miller are with the Illinois Hazardous Waste Research and Information Center (HWRIC), Champaign, IL 61820. Paul Randall is the EPA Project Officer (see below). The complete report, entitled "Evaluation of Ultrafiltration to Recover Aqueous Iron Phosphating/Degreasing Bath," (OrderNo. PB93-221 638/AS; Cost: $19.50, subject to change) will be available only from: National Technical Information Service 5285 Port Royal Road Springfield, VA 22161 Telephone: 703-487-4650 The EPA Project Officer can be contacted at: Risk Reduction Engineering Laboratory U.S. Environmental Protection Agency Cincinnati, Ohio 45268 United States Environmental Protection Agency Center for Environmental Research Information Cincinnati, OH 45268 Official Business Penalty for Private Use $300 BULK RATE POSTAGE & FEES PAID EPA PERMIT No. G-35 EPA/600/SR-93/144 ------- |