United States
Environmental Protection
Agency
Risk Reduction
Engineering Laboratory
Cincinnati, OH 45268
Research and Development
EPA/600/SR-93/144    September 1993
Project  Summary
 Evaluation  of  Ultrafiltration  to
 Recover Aqueous  Iron
 Phosphating/Degreasing  Bath
Gary D. Miller, Timothy C. Lindsey, Alisa G. Ocker, and Michelle C. Miller
  Pollution prevention efforts studied in
the report summarized here targeted the
hazardous waste generated from a 5000-
gal iron phosphating/degreasing bath used
by a metal fabricator to clean and precon-
dition steel parts for  painting. When oil
buildup in the bath began to sacrifice prod-
uct quality and the discharge levels of oil
and grease in the rinse water edged closer
to the maximum allowable limit, all 5000
gal were dumped and replaced. Periodic
dumping, about three times each year,
resulted in at least 15,000 gal/yr of hazard-
ous waste. Several waste minimization al-
ternatives were considered, and ultrafiltra-
tion was selected as the most promising
technology to recover and reuse the bath
and to reduce the total amount of hazard-
ous waste generated.
  This project  was carried  out in four
stages: (1) initial assessment of the prob-
lem  and evaluation  of  alternatives, (2)
bench-scale screening  of Ultrafiltration
membrane candidates, (3) pilot-scale study
at the Illinois Hazardous Waste Research
and Information Center (HWRIC), and (4)
full-scale implementation and testing
onsite at the company's facility. Full-scale
testing integrated the new waste reduc-
tion scheme into the facility's production
process by applying Ultrafiltration directly
to the  5000-gal  iron phosphating/
degreasing bath. Ultrafiltration success-
fully  removed oil contamination from the
bath  and returned clean process solution
back to the original 5000-gal tank. Ultrafil-
tration concentrated the hazardous com-
ponent down to 10 gal of oily waste and
reduced  hazardous  waste generation
99.8%. Permeate flux rates were  high
enough to compete with the constant in-
put of oil from the production line, and
concentrations of oil in the bath were main-
tained at acceptable operating levels. The
estimated payback period associated with
implementing Ultrafiltration was only 6.9
mo.
  This Project Summary was developed
by  EPA's  Risk Reduction Engineering
Laboratory, Cincinnati, OH, to announce
key findings of the research project that is
fully documented in a separate report of
the same title (see Project Report order-
ing information at back).

Introduction
  The objective of  the U.S. Environmental
Protection Agency  (EPA) and the Illinois
HWRIC was to evaluate potential technolo-
gies and operational modifications that could
reduce the amount of hazardous waste gen-
erated at a metal fabrication facility. The goal
of this project was to find an environmentally
responsible means to extend the life a 5000-
gal  iron  phosphating/degreasing bath and
thereby reduce hazardous waste generation.
The relative feasibility of Ultrafiltration as well
as its capability to reduce waste generation
were assessed on an engineering and eco-
nomic basis. Results of this project were used
to justify installing a permanent Ultrafiltration
system  and operating practices that would
improve product quality.

Industrial Participant
  R.B. White, Inc., of Bloomington, IL, oper-
ates a  sheet metal fabrication facility that
manufactures  painted steel  shelving units.
Cold-rolled steel arrives at the plant from the
steel mill coated with mill oils to protect the
                                                ^Ci  Printed on Recycled Paper

-------
bare metal from corroding or staining during
storage and fabrication operations. During fab-
rication, coolants and lubricants are also ap-
plied to the metal working surface.  Before
being painted, the metal surfaces are cleaned
to remove the  mill  oils and metal working
fluids and then  preconditioned to bond well
with  the paint coating.  Fabricated parts are
cleaned and phosphated in a 5000-gal heated,
aqueous immersion tank and rinsed  with a
fresh water spray. The company previously
operated  separate   degreasing  and
phosphating tanks using trichbroethylene  in
the degreasing tank  and in 1985, switched  to
a  single-stage  aqueous  iron  phosphating/
degreasing system to improve worker safety
and reduce the generation of organic solvent
emissions  and  hazardous waste. Although
the switch  eliminated the risks and liabilities
associated with organic solvents, it introduced
a new waste disposal problem.

Problem Description
   Simultaneous degreasing and phosphating
in  the same bath formed an oil-water emul-
sion. With extended  use, the buildup of oil  in
the bath  reduced cleaning and phosphating
efficiency, and product  quality was compro-
mised.  Additionally,  dragout  of oil from the
bath into the rinse water eventually pushed
oil and grease levels in the discharge over
the allowable limit. In the past, oil skimmers
were used to control oil slicks on the surface
and prolong the life of the bath, but the skim-
mers were only partially effective. When oil in
the bath began to sacrifice  product  quality
and the discharge levels edged closer to the
maximum allowable  limit, the bath had to be
replaced. Depending on production rates, the
bath typically lasted 3 to 4 mo. Replacing the
bath required a full day of lost production time
to take the process off-line,  make  arrange-
ments with a waste  transporter to drain and
dispose of the entire contents, and recharge
the tank with 5000 gal of fresh water and raw
materials.  The  spent bath was classified as
RCRA  hazardous waste  because it failed
Toxicrty Characteristic  Leaching  Procedure
(TCLP) tests for xylene. Since land disposal
of liquid wastes is prohibited, the bath, sludge,
and skimmed oil were  incinerated  in a ce-
ment kiln. Disposal costs  including transpor-
tation and incineration ran about $1/gal which
came to $5000/bath, or about $15,000/yr  in
addition to the costs  associated with lost pro-
duction time and replacement of water and
raw materials.

Process Background
   Iron phosphating/degreasing processes are
widely used in the manufacture of metal prod-
ucts  to clean and precondition ferrous  sur-
faces. Many metal fabricators and others that
paint or coat steel choose iron phosphating/
degreasing processes  because they effec-
tively clean metal parts, provide an excellent
surface for paint adhesion, and protect against
under-paint corrosion. The goals and mecha-
nisms  associated with the degreasing and
phosphating process are discussed bebw.
  The goal of degreasing is to remove mill
oils,  metal working fluids, and any other shop
soils from the steel surface and prepare it for
finishing. Degreasing was accomplished us-
ing nonbnic surfactants in a  heated (140°F),
air-agitated bath. The surfactants surrounded
the oil  and dirt particles and formed a stable
emulsbn that cleaned the  parts  and  pre-
vented the oil and dirt from  redepositing on
the metal surface.
  Phosphating is a common type of pre-
paint coating process used to simultaneously
provide corrosion  resistance and  enhance
paint adhesion to a metal surface. Phosphate
salts chemically bond to the metal surface to
produce an  amorphous  conversbn coating.
The  phosphate conversbn coating is  non-
conductive  so it protects the metal surface
from electrochemical oxidation that leads to
rust  and corrosbn. The  matrix of the phos-
phate coating forms capillaries that increase
the  surface area  and  provide a mechanical
interlocking structure on which the paint can
adhere.
  The 5000-gal bath was charged with Dura-
Gard Soke and Tart liquid acid (supplied by
DuBois Chemicals),* which contained  non-
ionic surfactants, phosphate salts, phosphorb
acid, and accelerators to promote phosphate
precipitation. The concentratbn of Dura-Gard
Soke and the pH in the bath were checked
daily with a  simple titration  kit  and  litmus
paper  to ensure  that concentrations  were
maintained between 1.5  and 2.0 oz Dura-
Gard/gal and at a pH of 3.5.

Waste Reduction in the Metal
Fabricated Products Industry
  The EPA's campaign  for waste  reduction
is bringing change to industries through the
1984 Hazardous  and Solid Waste Amend-
ments (HSWA) to RCRA, the Toxics Release
Inventory (TRI), the 1990 Pollution Preven-
tion Act (PPA), and the more recent 33/50
Program. The HSWA require industries to set
up waste minimization programs and to pro-
duce certified  manifests  demonstrating  their
waste reduction efforts. The TRI is a comput-
erized data base that tracks the routine and
accidental release of approximately 300 toxic
chemicals reported  by U.S.  manufacturers.
The  1990  PPA brought  about stricter TRI
industrial report requirements that include pro-
viding information on pollution prevention ef-
forts. The 33/50 Program is EPA's voluntary
"Mention of trade names or commercial products does
 not constitute endorsement or recommendation for
 use
pollution  preventbn initiative to reduce  the
Natbn's releases of 17 TRI chemicals 33%
by the end of 1992 and 50% by the end of
1995. Backed by federal legislatbn and eco-
nomic incentives,  EPA's pollutbn preventbn
campaign has targeted several operatbns
associated with the metal fabricated products
industry. Finding environmentally responsible
solutions to the industry's waste disposal prob-
lems  has focused on source reductbn  (in-
cluding process modifications and raw mate-
rials substitution) and recycling.
  The EPA recommends various strategies
for pollution prevention in the metal fabricated
products  industries. Until now, waste reduc-
tion in surface preparation operations  has
focused on conserving or finding alternatives
to organic solvent cleaners. For years,  the
metal finishing industry has  relied on organic
solvents for cleaning metal parts. Trichbroet-
hylene, methylene chloride, perchloroethyl-
ene, and  1,1,1-trichloroethane account for a
majority of the chbrinated solvents used by
industry.  Recently, however,  environmental
concerns  for  health and  disposal conse-
quences have increased. Chbrinated solvents
were not only targeted by the TRI and 33/50
Program, but solvent wastes were among the
first to be banned from land disposal by  the
1984  HSWA.   More   recently,   1,1,1-
trichloroethane has been  linked  to  ozone
depletion in the upper atmosphere and will no
longer be manufactured in the U.S. after 1995.
As restrictbns increased the cradle-to-grave
liability for solvent waste generators, the metal
finishing industry began to turn  to other  op-
tions for cleaning operations. Aqueous clean-
ers, emulsion cleaners, mechanical and ther-
mal methods, and abrasive cleaners emerged
as alternatives to organb  solvents.  These
optbns help reduce emissions of volatile or-
ganb compounds (VOCs) and lessen worker
exposure. The switch to aqueous cleaners
can also reduce the annual reporting required
under  SARA  Title  III,  Section 313, Toxic
Chemical Release Reporting:  Community
Right-To-Know.
  Aqueous cleaners have already replaced
solvent degreasers in many  industrial surface
preparation  operations.  The  water-based
cleaners  effectively remove protective  oils,
cutting oils, hydraulic fluids,  silbone oils, wa-
ter soluble coolants, shop dirts, finger prints,
and other soils. Special additives also make
the aqueous cleaners versatile coating solu-
tbns.  Making the switch  has  even made it
possible  to  eliminate some  separate
degreasing and coating processes as well as
reduce waste generation. Aqueous cleaners
are finding success in many  industrial surface
preparation operatbns including airplane com-
ponents, printed circuit boards, advanced com-
posites, fasteners, and automotive parts.
  The tank  life of the aqueous cleaners is
limited by the buildup of the dirts and oils in

-------
the bath.  Cleaning effectiveness begins to
deteriorate,  and the performance of other
chemicals in the bath is  inhibited. Although
the aqueous degreasers do not carry all the
risks and  liabilities associated with the dis-
posal of waste organic solvent cleaners, peri-
odic replacement of the bath creates a differ-
ent waste disposal  problem.
  Current disposal  options for spent aqueous
cleaning solutions include tankering, incinera-
tion, or discharge.  The rising costs associ-
ated with these disposal and pollution control
options are the main incentives to extend the
life of the aqueous cleaner baths. Rather than
wasting valuable raw materials, the aqueous
cleaners have the potential to  be recycled
again and again. Depending on the physical
characteristics of the bath solution, the life of
the bath can be extended by skimming con-
taminants  off the top, settling heavier frac-
tions to the bottom, or filtering out suspended
species.

Ultrafiltration
  Conventional filtration techniques rely on
depth or screen filters to remove oil and dirt
from a process solution, but conventional fil-
ter media  clog easily. They require frequent
backflushing or disposal, which result in addi-
tional wastes.  Membrane filtration is a more
advanced  technique that takes advantage of
thin-film membranes and turbulent flow pat-
terns to deliver a more consistent flow rate
and a higher quality filtrate than conventional
filtration. Ultrafiltration is one class of mem-
brane  filtration that uses  membranes  with
pore diameters ranging from 10'9 to 1Q-6 m.
  The  Ultrafiltration  process works by produc-
ing  two separate streams: concentrate and
permeate. The permeate stream contains
only the components in the feed solution
small enough to pass through the membrane
pores (water, solubilized species). The con-
centrate stream contains everything else that
is rejected by  the membrane  (emulsified oil
and dirt).
  The  recent development of more durable
membranes, such  as PVDF, has expanded
the application of Ultrafiltration  beyond its ori-
gins in the food industry to successfully handle
industrial process solutions with extreme pHs,
high temperatures, and high  oil concentra-
tions.  Because of  its  unique  capabilities to
concentrate  oily wastewater and produce a
clear filtrate, Ultrafiltration has emerged as a
promising technology for extending the life of
aqueous cleaner baths. Ultrafiltration of oil-
water emulsions is a more straightforward
method for  removing  and concentrating oil
than are other physical, chemical, or thermal
means. Ultrafiltration does not require a stock-
pile of  chemicals and does not produce a
chemical sludge that requires special treat-
ment or disposal. Instead, Ultrafiltration pro-
duces a water phase that requires no further
treatment and a concentrated phase only a
fraction of the original volume that can sus-
tain combustion or be disposed of efficiently.
Ultrafiltration requires no heat input, low en-
ergy, and little operator attention.
  One of the greatest limitations of Ultrafiltra-
tion membranes  is their tendency to foul.
Fouling  is detected as the decrease in per-
meate flux over time, where the flux is de-
fined as the volumetric flow rate of permeate
per cross-sectional area per time. Fouling is
mainly due to the accumulation  of particles
on the membrane surface and/or within the
pores of the membrane itself.  In  industrial
applications where Ultrafiltration could be used
to filter aqueous cleaning  baths, fouling will
typically  be  due to oils, suspended  solids,
free surfactants, and metal precipitates. When
a membrane shows signs  of fouling, the flux
can largely be restored by cleaning the mem-
brane, but a portion of the flux may be unre-
coverable because of irreversible fouling.

Full-Scale Testing
  Results from the bench- and  pilot-scale
studies were used to develop  a full-scale,
modified-batch test conducted onsite at the
facility. Figure 1 shows how the full-scale test
applied Ultrafiltration directly to the 5000-gal
iron phosphating/degreasing bath. The objec-
tive was to  directly  measure the effect of
Ultrafiltration  on the process solution  under
actual plant conditions. The full-scale test took
into account the constant input of oil from the
production line and the daily addition of bath
chemicals. Additionally, the full-scale test also
helped identify problems with the Ultrafiltration
equipment and anticipate changes that should
be made on a permanent unit.
  The full-scale in-plant testing  featured an
Ultrafiltration system provided by Koch Mem-
brane Systems (Model UF-4)  equipped with
four 1-in tubular PVDF membranes (100,000
                        Concentrate
       Pump
ffrr
                                Men brane
                             Permeate to bath
Figure 1. Modified-batch scheme Ultrafiltration.
MWCO,  4.4 sq ft total area). Data obtained
from the full-scale modified-batch  test was
used to determine whether Ultrafiltration would
be a viable option for waste reduction at the
plant. Technical, operational, and economic
aspects associated with the Ultrafiltration equip-
ment were examined to evaluate the feasibil-
ity of this technology to improve the company's
metal fabrication operation.
  When  field testing  began,  the  iron
phosphating/degreasing bath had not been
replaced in over 3 mo. The aqueous solution
was murky with dirt and oil, and large patches
of free oil floated on the surface. The changes
that took place  over the next 11  days of
Ultrafiltration testing produced a dramatic ef-
fect. Surface oil slicks disappeared and were
replaced by a clean, light  foam.  The  bath
solution was visibly clearer, and plant person-
nel  testified that it looked like a freshly re-
charged bath. Results of total organic carbon
(TOC)  analyses  for  the full-scale testing
showed the change in oil and surfactant con-
centrations during the test (Figure 2).

Economic Analysis
  The  costs  and benefits  associated  with
installing an Ultrafiltration system were  ana-
lyzed to determine the economic feasibility of
this technology. Based on the estimated ex-
penditures and savings, the payback period
associated with this technology, was only 6.9
mo. The net present value and interest rate of
return indices were $152,143 and  178%, re-
spectively. Therefore, investment in an ultra-
filtration system represented a very attractive
economic alternative.

Conclusions
  The  overall evaluation of this pollution pre-
vention project was  based  on Ultrafiltration
performance, product quality, and  econom-
ics.  Results indicated that the concentration
of oil in the iron phosphating/degreasing bath
was substantially reduced and maintained at
acceptable operating  levels.  Virtually all of the
unused phosphating agents were conserved
although a portion of the unused surfactants
was not. Permeate rates exhibited excellent
performance during the acidic (pH=3.5), high
temperature (140°F) operation and were high
enough to process the constant input of oil
from the production line. The entire 5000-gal
bath was processed in 180 Ultrafiltration oper-
ating hours.  Coating weight, rust creepage,
and paint adhesion tests conducted by DuBois
Research Laboratory and plant personnel on
samples  of steel parts indicated that product
quality  achieved during the full-scale study
was good for the plant's  application.  The
payback period for implementing the Ultrafil-
tration  system was 6.9 mo. By using Ultrafil-
tration, the company will reduce its hazard-
ous waste generation by at  least 15,000 gal/
yr, a 99.8% reduction.
         £l).S. GOVERNMENT PRINTING OFFICE: 1993 - 7«NMm/moS9

-------
   300
       ,
   200 -1
O
   roo
             Increased surfactant
             due to increased
             Dura-Gard additions
                           'Surfactant

                                 Oil
       0             100          200

            Operating Time (hours)
 Figure 2. Oil and surfactant in bath vs time.
  This project has successfully demonstrated
the ability of membrane filtration to reduce
hazardous waste generation and recover valu-
able raw materials in a metal fabrication op-
eration. This application introduces another
innovative waste reduction technique to the
metal fabricated products industry that could
benefit the many plants nationwide that use
aqueous cleaner  systems  like  the iron
phosphating/degreasing process at the R.B.
White company. The  ultrafiltration system
implemented in this project saves money,
maintains good product quality, and reduces
waste generation.
   G.D. Miller, T.C. Lindsey, A.G. Ocker, and M.C. Miller are with the Illinois
     Hazardous Waste Research and Information Center (HWRIC), Champaign,
     IL 61820.
   Paul Randall is the EPA Project Officer (see below).
   The complete report, entitled "Evaluation of Ultrafiltration to Recover Aqueous
       Iron Phosphating/Degreasing Bath," (OrderNo.  PB93-221 638/AS; Cost:
       $19.50, subject to change) will be available only from:
           National Technical Information Service
           5285 Port Royal Road
           Springfield, VA 22161
           Telephone: 703-487-4650
   The EPA Project Officer can be contacted at:
           Risk Reduction Engineering Laboratory
           U.S. Environmental Protection Agency
           Cincinnati, Ohio 45268
     United States
     Environmental Protection Agency
     Center for Environmental Research Information
     Cincinnati, OH 45268

     Official Business
     Penalty for Private Use
     $300
                                                         BULK RATE
                                                   POSTAGE & FEES PAID
                                                             EPA
                                                       PERMIT No. G-35
     EPA/600/SR-93/144

-------