United States
                     Environmental Protection
                     Agency
Risk Reduction
Engineering Laboratory
Cincinnati, OH 45268
                     Research and Development
EPA/600/SR-93/160    September 1993
i&EPA       Project Summary
                     Recycling  Nickel  Electroplating
                     Rinse  Waters by  Low
                     Temperature  Evaporation  and
                     Reverse Osmosis
                     Timothy C. Lindsey
                       Low temperature evaporation and re-
                     verse osmosis systems were each
                     evaluated  (on a pilot scale) on their
                     respective ability to process rinse wa-
                     ter collected from a nickel electroplat-
                     ing operation. Each system offered ad-
                     vantages under specific operating con-
                     ditions.  The low temperature evapora-
                     tion system was best suited to pro-
                     cessing solutions  with relatively high
                     (greater than 4,000 to 5,000 mg/L) nickel
                     concentrations.  The reverse osmosis
                     system was best adapted to conditions
                     where the feed solution had a relatively
                     low (less than  4,000 to  5,000 mg/L)
                     nickel concentration. In electroplating
                     operations where relatively dilute rinse
                     water solutions  must be concentrated
                     to levels acceptable for replacement in
                     the plating bath, a combination of the
                     two technologies might provide the best
                     process alternative. Initially, the reverse
                     osmosis system could be used to con-
                     centrate the feed solution. This could
                     be followed by low temperature evapo-
                     ration processing  to  concentrate the
                     solution to levels acceptable for re-
                     placement in the plating bath.
                       This Project Summary was developed
                     by EPA's Risk Reduction Engineering
                     Laboratory, Cincinnati, OH, to announce
                     key findings of the research project
                     that is fully documented in a separate
                     report of the same title  (see Project
                     Report ordering information  at back).

                     Introduction
                       This project was  a joint  effort of Gra-
                     ham Plating, Chicago, IL, an  electroplat-
ing firm; the Hazardous Waste Research
and Information Center (HWRIC), a divi-
sion of the Illinois Department of Energy
and Natural Resources, Champaign, IL;
and the  Pollution Prevention Research
Branch of the U.S. Environmental Protec-
tion Agency's Risk Reduction Engineering
Laboratory,  Office of Research  and De-
velopment, Cincinnati, OH.
  Graham Plating is a  large "job-shop"
that has been located for many years on
the  northwest side of  Chicago.  A new
modern building has recently been com-
pleted in Arlington Heights, IL, and Gra-
ham  Plating currently plans  to relocate
the plating operations to the new facility.
This new facility has been designed and
constructed such that special features have
been installed to  promote  waste reduc-
tion. Large  underground rinse water col-
lection tanks have been installed to facili-
tate accumulation, segregation, and stor-
age of  rinse  waters by principal metal
component. This water can subsequently
be treated through a reverse osmosis sys-
tem, a low temperature evaporation unit,
or both.
  This project was performed to evaluate,
compare, and  document the effectiveness
of low temperature evaporation and re-
verse osmosis technologies for recovery
and reuse of water and plating bath chemi-
cals associated with electroplating  rinse
waters. These technologies were exam-
ined on a pilot scale at the HWRIC pilot
laboratory facility  by  using  actual  rinse
water samples collected from a Graham
Plating nickel electroplating line. Economic
assessments  conducted for these tech-
nologies assumed that 7,200 gal of nickel
                                                                   \£) Printed on Recycled Paper

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electroplating rinse water would  have to
be processed per day at this facility on a
5-day week and 80% availability basis.


Technology Descriptions
  Low temperature evaporators (Licon,
Inc., Pensacola,  FL)* heat water  under a
vacuum to produce steam at relatively low
* Mention of trade names or commercial products does
 not constitute endorsement or recommendation for
 use.
temperatures (150 to 160° F). The steam
rises into a condenser where distilled wa-
ter results. The plating bath chemicals do
not rise with the steam  and become a
concentrated slurry or solution of chemi-
cals. The evaporation unit is a model C-3,
single effect, pilot-scale evaporator espe-
cially designed for conducting pilot-scale
tests on a variety of feed solutions. Figure
1 provides a schematic of material flow
through a  low temperature evaporation
system.
  Reverse  osmosis is a pressure-driven
membrane  separation process in which a
feed stream under pressure (200 to 800
psi) is separated into a purified "perme-
ate" stream and a "concentrate" stream by
selective permeation of solution through a
semi-permeable membrane. The pressure
required  to force the permeate through
the membrane is dictated by the osmotic
pressure of the feed stream. Membranes
are constructed  of a variety of  materials
such as aromatic polyamide, cellulose ac-
etate, and polyether/amide. The reverse
osmosis  unit used in this project was an
Osmonics  Model  PES/OSMO-19T-
80SSXXC reverse osmosis machine for
                           Cooling
                           Water
                           Outlet
                                                                                    Concentrate
                                     Feed/Concentrate   (l_J

                                     Steam or Hot Water Qj

                                     Distillate           \3j

                                     Cooling Water      ^J
   Figure 1.   Basic flow diagram for single effect evaporator.

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       Feed In
               permeate
               Spacer     Membrane   Feed Spacer
Figure 2.   Components of a spiral-wound membrane.
process evaluation. It was equipped with
one Osmonics Model Number 192T-MSO5
thin-film,  composite, spiral-wound mem-
brane cartridge. Figure 2 provides a view
of the components that comprise a spiral
wound  membrane. The solution was
prefiltered through a 5 u cartridge filter for
the reverse osmosis testing.
  Four, 55-gal drums of nickel electroplat-
ing rinse water were collected from the
Graham  Plating facility  and  processed
through the low temperature evaporation
(Drums A and B) and the reverse osmosis
(Drums C and D) systems.  The  reverse
osmosis tests were conducted at two dif-
ferent  operating pressures: Drum  C at
pressures of 250 to 300  psi and  Drum D
at 350 to 380 psi. Samples of the concen-
trated feed solution as well  as the  distil-
late (low temperature evaporation  system)
and permeate  (reverse osmosis  system)
were collected at regular intervals through-
out the tests as the rinse water was pro-
cessed. Nickel analyses were done to de-
termine how efficiently the  systems  re-
moved nickel from the  rinse  water and
concentrated it for potential  recycling.
Analyses for total organic carbon (TOG)
were done to indicate  the fate of organic
constituents (e.g., brighteners)  in the rinse
water. Immediately after samples  were
collected, electrical conductivity measure-
ments were made to indicate the soluble
salts present in the samples.


Low Temperature Evaporation
System Efficiency
  The low temperature evaporation sys-
tem exhibited consistent  productivity
throughout the tests. This performance fea-
ture was unfailing regardless of the chemi-
cal concentrations of the feed solution pro-
vided to the system. The evaporation sys-
tem concentrated the  rinse water, which
had exhibited initial nickel concentrations
of 2,540 to 4,140 mg/L to nickel levels as
high as 13% to 18%. These levels are
well above the 8% required for placement
into the plating bath. The concentrate, per-
meate, and distillate nickel concentrations
exhibited in samples collected throughout
the tests have been  summarized (Table
1).  Figure 3  shows  how  nickel levels
changed in the feed solution during the
course of the low temperature evapora-
tion tests. Nickel concentrations increased
at a steady rate  until concentrations  of
approximately 25,000 to 30,000 mg/L were
reached. This level corresponds to a point
where approximately 80%  to 85% of the
rinse water volume had been processed.
Beyond this point, nickel concentrations
increased dramatically until the final con-
centrations  of  13% and  18% were
achieved. The rinse water feed  solution
volume  was reduced  by over 98% as a
result of this  process. The evaporation
system concentrated the organic constitu-
ents of  the rinse water  from initial TOC
levels of 550 to 990 mg/L to final levels of
25,000 to 26,000 mg/L. TOC levels in the
Graham Plating nickle baths are normally
maintained at approximately 14,000 mg/L.
The concentration rate of the organic com-
ponents paralleled the nickel concentra-
tion rate suggesting that little of the or-
ganic material was lost to volatization. As
shown in  Table 2, distillate produced by
the low temperature evaporation system
was very low in nickel concentration (av-
erage  0.37 to  0.71  mg/L).  Additionally,
TOC concentrations in the distillate were
very low (average 3.04 to 3.50 mg/L).
  Disadvantages of the  low temperature
evaporation system include its  relatively
high ($140,000) capital cost and high en-
ergy  requirements  ($20/1,000  gal  pro-
cessed).  The  implied rate of return of
10.6% and payback period of 6.9 yr deter-
mined in the economic assessment for
this system suggest that it is  a  marginal
investment  opportunity by today's  stan-
dards. These estimates do not, however,
consider the  reduced future liabilities
brought about by  drastically  decreasing
the hazardous waste discharges from the
facility.

Reverse Osmosis System
Efficiency
  The feed  solution processed through
the reverse osmosis system contained ini-
tial nickel concentrations of 1,425 to 2,580
mg/L (Table 1). Figure 4 depicts how nickel
concentrations  in the  feed  solution
changed as the solutions were processed.
Nickel concentrations  increased steadily
until about 60% of the  rinse water volume
was processed. At this point,  nickel  con-
centrations were about 4,000 to 5,000
mg/L  in the two drums. Beyond this point,
nickel concentrations increased more rap-
idly until final concentrations of 12,560
mg/L  (Drum C) and 17,900 mg/L (Drum
D)  were reached.  The reverse osmosis
system exhibited superior productivity at
the beginning of the tests, and productiv-
ity  dropped  off dramatically  after about
60%  of the feed solution had been pro-
cessed. Beyond these levels,  the produc-
tivity  of the  reverse osmosis equipment
decreased dramatically as solids began to
precipitate and foul the membrane. The
final concentrations achieved  with the re-
verse osmosis process were 12,560 to
18,200 mg/L (1.256% to 1.82%) and are
well below the 8% nickel concentration
required for the plating bath. Some of this
solution could be  used to replace water
losses in the electroplating process. The
reverse osmosis system, however, would
probably produce excess volumes of con-
centrated rinse water  composed of 1.2%
to 1.8% nickel. This material  would  have
to be  further processed with the use of an
alternative technology such as  low  tem-
perature evaporation  or be shipped to  a
facility that could extract the nickel for use
in other industrial processes.
   The reverse osmosis system concen-
trated the organic constituents present in
the rinse water feed  solution from initial
TOC  levels of 340 to 540 mg/L to levels of
2,800 to 3,500 mg/L. These concentra-
tions  suggest that the organic bath con-
stituents are concentrated by  the reverse
osmosis equipment at rates that parallel
the nickel concentration rates.
   The quality of the cleaned  rinse  water
permeate produced by the reverse osmo-
sis equipment was directly related to the

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 Table 1.  Comparison of Nickel Concentrations in Concentrate, Distillate, and Permeate
 Product
                             Low Temp. Evap.                   Reverse Osmosis
                          Drum A         Drum B          Drum C          Drum D
 Concentrations at beginning of test (mg/L):
   Concentrate              4,140
   Distillate                  2.5
   Permeate                  —

 Concentrations at end of test:
   Concen tra te             179,000
   Distillate                   1
   Permeate                  —

 Ratio of distillate permeate to concentrate:
   Distillate
   Permeate
                          0.02%
                                         2,540
                                         2.2
                                         128,000
                                         0.3
                                         0.01%
2,580
44.5
12,560
210
1,425
14.5
18,200
790
                                                          1.49%
                                                                          1.54%
    200000
    100000  -
                                                                       o Drum A
                                                                       * Drum B
                    20
                              40         60         80


                          % of Drum Volume Processed
                                                                i
                                                              100
Figure 3.
          Concentrate nickel concentration versus percent of drum volume processed;
          low temperature evaporation tests.
quality of the feed solution pumped into
the unit. Permeate produced by  the  re-
verse osmosis system averaged 89 to 134
mg/L nickel (Table 2). These  levels are
about 98.5% lower than the nickel con-
centrations present in the concentrated
solution. This  solution would  not,  how-
ever, be acceptable for discharge  to pub-
licly  owned treatment works. The nickel
levels present in this solution  could  be
further reduced  by passing this solution
through the reverse  osmosis equipment
again. TOG concentrations averaged 19.46
                                          to  21.98 mg/L in the permeate  solution
                                          which suggests that some of the organic
                                          compounds were able to permeate the
                                          membrane. The  reverse  osmosis equip-
                                          ment condensed the feed solution to final
                                          volumes that were 88% to 94% less than
                                          the original volumes  of  the two tested
                                          drums. Differences between the two tests
                                          can be attributed to the difference in oper-
                                          ating pressures used during the tests.
                                            Advantages of the reverse osmosis sys-
                                          tem include its relatively  high production
                                          rates with respect to low concentration
 feed solutions.  Additionally, it would re-
 quire  lower capital investment  (about
 $50,000) than a comparably sized low tem-
 perature evaporation system. Energy costs
 required to operate a reverse osmosis sys-
 tem would be only about $2.50/1,000 gal
 processed. Disadvantages associated with
 a reverse osmosis system include its in-
 ability to concentrate the feed solution to
 levels beyond the 12,560 to 18,200 mg/L
 levels revealed  in this study.  This factor
 alone would prevent use of a stand-alone
 reverse  osmosis system at the Graham
 Plating facility because  of the economic
 impracticalities associated with the  con-
 centrate produced by the system. Another
 disadvantage associated with the reverse
 osmosis system  is the lower quality per-
 meate produced by the system. This solu-
 tion would probably  have to  be  reused
 within the  plant or further  processed
 through  the reverse osmosis system be-
 fore discharge to the POTW.

 Combined Use
   Both the  low  temperature evaporation
 and reverse  osmosis systems  appear to
 offer advantages under specific operating
 conditions. Based on this factor, the po-
 tential for utilizing these technologies  in
 tandem  was examined. The reverse os-
 mosis  system is best adapted to condi-
 tions where the  feed solution has  a rela-
 tively low nickel concentration. It can pro-
 cess the low concentration feed solution
 with relatively high efficiency to a level of
 4,000  to 5,000  mg/L. At this  point, the
 solution could be transferred to a low tem-
 perature evaporator for further concentra-
 tion. The low temperature evaporation sys-
 tem appears to  be best  adapted to  pro-
 cessing solutions with relatively high nickel
 concentrations. It can process these solu-
 tions so  that a concentrate solution com-
 posed  of 8% or more nickel is produced
 along with a very high-quality distillate so-
 lution. Using the equipment within its opti-
 mum operating ranges would augment the
 ability of the systems to process the rinse
 water with maximum efficiency while sup-
 plying  the  electroplating operation with
 high-quality concentrate, distillate, and per-
 meate solutions for reuse. Since the equip-
 ment would always be functioning within
 optimum concentration ranges,  smaller re-
 verse osmosis and low temperature evapo-
 ration units could be implemented than if
the individual units were used alone.  If
this  type of combined system were in-
 stalled at the Graham Plating  facility,  it
would  require  a capital  investment of
$115,000, which  would  be paid back in
2.8 yr  through  a 27.6% implied  rate of
 return.

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Electrical Conductivity

  Electrical conductivity  measurements
taken during operation of both the low
temperature evaporation and reverse os-
mosis systems could be of  great value
during  actual plant operating conditions.
The  electrical conductivity data obtained
in this project were well  correlated  with
nickel concentration, TOC concentration,
and membrane flux characteristics. Accu-
rate  assumptions regarding concentrate,
permeate,  and  distillate quality could be
based on electrical conductivity measure-
ments taken throughout the work day. Fur-
ther, the equipment could be automated
to accumulate and discharge the  various
solutions based on  in-process electrical
conductivity measurements that could ac-
tivate pumps, valves, and/or switches when
preset levels were attained.


Additional Research Needs
  Additional tests need to be conducted
with rinse water from other electroplating
lines involving other metals. These tests
would aid in determining the usefulness of
these technologies with respect  to  pro-
cessing the entire spectrum of rinse water
streams that would be produced at a full-
scale electroplating  operation. Detailed
analysis of  all organic and inorganic rinse
water components  (organic brighteners,
sulfate, chloride, etc.) would be  useful to
determine the effects of low temperature
evaporation and reverse osmosis process-
ing on the relative quality  and quantity of
these constituents. Onsite testing should
be  done at  an electroplating facility  to
allow comparison of full-scale systems with
the pilot-scale tests performed in this study.
This onsite testing would include detailed
study of the performance  of the concen-
trated  rinse water that is  returned to the
plating bath.
  The full report  was submitted in fulfill-
ment of Contract  CR-815829 by Hazard-
ous Waste Research and Information Cen-
ter under the sponsorship  of the  U.S. En-
vironmental Protection Agency.
 Table 2. Average Nickel Concentrations in Distillate and Permeate
                                 Distillate Ni Concentration
                                                                                Permeate Ni Concentration



A (n=13)
B (n=16)
C (n=22)
D (n=17)

Mean
(mg/L)
0.71
0.37
—
—
Standard
Deviation
(mg/L)
0.63
0.52
-
—

Mean
(mg/L)
—
—
89.55
134.38
Standard
Deviation
(mg/L)
	
—
49.22
202.19
                    20000  -i
                     10000
                                                        Drum C
                                                        Drum D
                                     20          40          60
                                            % of Drum Volume Processed
                               80
                                            100
Figure 4.   Concentrate nickel concentration versus percent of drum volume processed; reverse osmosis tests.
          •&V.S. GOVERNMENT PRINTING OFFICE: H*3 - 750-071/H006I

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Timothy C. Lindsey is with the Hazardous Waste Research and Information
  Center, Champaign, IL 61820.
Paul Randall is the EPA Project Officer (see below).
The complete report, entitled "Recycling Nickel Electroplating Rinse Waters by
    Low Temperature Evaporation and Reverse Osmosis," (Order No. PB93-
    218865; Cost: $19.50, subject to change) will be available only from:
       National Technical Information Service
       5285 Port Royal Road
       Springfield, VA 22161
        Telephone: 703-487-4650
The EPA Project Officer can be contacted at:
       Risk Reduction Engineering Laboratory
       U.S. Environmental Protection Agency
       Cincinnati, Ohio 45268
  United States
  Environmental Protection Agency
  Center for Environmental Research Information
  Cincinnati, OH 45268

  Official Business
  Penalty for Private Use
  $300
     BULK RATE
POSTAGE & FEES PAID
         EPA
   PERMIT No. G-35
  EPA/600/SR-93/160

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