United States
                     Environmental Protection
                     Agency
Risk Reduction
Engineering Laboratory
Cincinnati, OH 45268
                     Research and Development
EPA/600/SR-93/223    February 1994
&EPA       Project  Summary

                     Ultrasonic  Cleaning as a
                     Replacement for a
                     Chlorofluorocarbon-Based
                     System
                     P. B. Kranz, T. Gardner-Clayson, K. C. Malinowski, T. D. Schaab,
                     J. E. Stadelmaier, and P. M. Randall
                       The study summarized here evalu-
                     ated, on a technical and economic ba-
                     sis, the replacement of a solvent vapor
                     degreasing system using chlorofluoro-
                     carbons (CFC-113) with an  ultrasonic
                     cleaning system using a heated water-
                     based cleaning fluid for cleaning stain-
                     less steel parts.
                       The intent of the substitution was to
                     reduce fugitive volatile emissions while
                     eliminating the use and handling of haz-
                     ardous materials at the facility. The ul-
                     trasonic cleaning system was custom
                     fabricated to meet the dimensions re-
                     quirements of the parts fabricated on
                     site.  Cleaning standards for the  new
                     system were to remain consistent with
                     the criteria used for vapor degreasing.
                       Through  the utilization of an ultra-
                     sonic cleaning system,  fugitive emis-
                     sions have been significantly curtailed.
                     Volatile emissions are estimated to be
                     reduced 68% (3,450  vs. 10,876 Ib/yr)
                     over  the period  1990 to 1992. This re-
                     duction was in addition to the elimina-
                     tion of bench top freon cleaning units
                     at the facility, which reduced emissions
                     from  25,215 to 10,876 Ib/yr  from 1987
                     to 1990. The elimination of 26 drums/yr
                     of still bottoms generated through sol-
                     vent reclamation was also realized.
                       To  complete the economic evalua-
                     tion,  the costs of raw material (clean-
                     ers), utilities, and labor was considered
                     along with waste disposal.  An annual
                     savings, utilizing the ultrasonic clean-
                     ing system, was projected to  be $27,875
                     with the most significant savings real-
                     ized with the cost differential in  raw
                     materials because of the high cost of
chlorofluorocarbon cleaning solvents.
A payback period of 1.6 yr was calcu-
lated for the project.
  Additional benefits from the emission
reduction include improved working en-
vironment, reduced indoor air pollut-
ants, and better community relations.
  This Project Summary was developed
by EPA's Risk Reduction Engineering
Laboratory, Cincinnati, OH, to announce
key findings of the research  project
that is fully documented in a separate
report of the same title (see  Project
Report ordering information at back).

Introduction
  The use of CFCs in  vapor degreasing
cleaning systems has been the accepted
standard  in various industries for many
years. This process has been universally
accepted because  of the efficiency and
ease with which parts  are cleaned and
the subsequent compliance with quality
control standards for cleanliness of the
parts or materials cleaned. In recent years,
however, the disadvantages of this tech-
nology have become increasingly appar-
ent — the process' generation of fugitive
emissions resulting in  reporting require-
ments under SARA Title  III, concerns about
employee health and safety, and increased
cost and  taxation of CFCs. Furthermore,
CFCs are targeted for  eventual elimina-
tion because of their ozone depleting char-
acteristics.
  The project objectives were to evaluate
the technical feasibility, performance, eco-
nomic impact, and reduction of  fugitive
volatile emissions resulting from the sub-
                                                                     Printed on Recycled Paper

-------
  stitution  of vapor  degreasing  with aque-
  ous ultrasonic cleaning.
    This is a study of the effectiveness and
  applicability of ultrasonic cleaning using a
  heated water-based  cleaner as a means
  to clean  stainless  steel components.  An
  evaluation was completed under the Erie
  County/EPA  WRITE Program as a joint
  effort by Conax Buffalo Corp., Cheektowaga,
  NY; Erie County Environmental Compliance
  Services, Buffalo, NY; Recra Environmen-
  tal,  Inc., Amherst, NY; and the U.S.  Envi-
  ronmental  Protection Agency,  Office of
  Research and  Development,  Cincinnati
  OH.

  Procedure
    The  industrial participant  for this pro-
  gram  was  Conax  Buffalo  Corporation
  (Conax).  Conax has been engaged in the
  design  and  manufacture of  highly engi-
  neered, precision products for industrial,
  aerospace,  nuclear, fiber optic, and  mili-
  tary applications. At Conax, stainless steel,
  aluminum and copper parts  coated  with
  standard screw oils, water-based coolants,
  inhouse shop dirt, and metal shavings are
  cleaned in a series of cleaning and rinsing
  tanks of modular design using a heated
  alkaline solution. Previously, cleaning ac-
  tivities involved  the use of two types  of
  freon-based solvents that generated more
  than 10,000 Ib of fugitive emissions annu-
  ally from  two  vapor degreasers and two
  work bench stations.
   Since 1990, chlorinated solvents  and
  chlorofluorocarbons (CFC-113) including
  trichloroethylene,  1,1,1-trichloroethane,
 trichlorotrifluoroethane (freon),  and a freon/
 acetone mixture have been used at Conax.
 The CFCs are used for both degreasing
 parts after machining, and cleaning parts
 prior to assembly, shipment, or stock.  Un-
 til recently, four  operations within Conax
 utilized chlorinated  solvents  and CFCs.
 These  include  machining centers parts
 cleaning, machine shop vapor degreasing,
 assembly vapor degreasing, and final as-
 sembly cleaning.
   Because of their ozone depleting char-
 acteristics, CFCs are  targeted for  even-
 tual elimination  per the  1987  Montreal
 Protocol and Clean Air Act. The costs of
 CFCs are increasing and the use of CFCs
 is going to  be taxed. Reclamation of CFCs
 generates  stillbottoms that are F002 haz-
 ardous waste. The ultrasonic parts clean-
 ing system was  installed  to  avoid and
 eliminate the problems associated with fur-
 ther CFC use.
  For 2  wk in January  1992, the  ultra-
 sonic cleaning system  was evaluated  for
 131 batches  of parts ranging  from  large
tubes to pins and from 1  to several thou-
sand parts/batch. Because this was con-
  sidered  typical production,  the results
  would be extrapolated to an annual basis.
  Average cleaning times and chemical ad-
  dition requirements were documented, and
  subjective quality control inspections were
  done on each batch. Project forms devel-
  oped for the project tracked the time in
  minutes for each batch  at each station in
  the cleaning process. Clean and rinse tank
  pH was  monitored  along with  the clean
  and heated rinse tank temperatures. The
  number and description of parts in each
  batch were also listed on another project
  form. Averages for processing times, pH,
  and temperatures were calculated along
  with totals  for a breakout  of batch  part
  quantities from 1 to  15,  15 to  100, 100 to
  1000 and 1000+ parts/batch.
    The batches of tubes cleaned during
  the monitoring period were totaled. The 8-
  ft-long tubes were  of particular interest
  due to the part configuration. To limit fugi-
  tive emissions, the surface area and work-
  ing  area of the  vapor degreasers were
  limited. This required a "double dip" pro-
  cedure for  cleaning the 8-ft-long tubes.
  Because  of the length of the tubes,  this
  procedure required an extended period of
  CFC use resulting in greater emission gen-
  eration. The ultrasonic cleaner was  de-
  signed to accommodate long  tubes in a
  "single dip" cleaning  operation eliminating
  the  emissions  and  facilitating smoother
  parts cleaning operation.
   The Miraclean* system used by Conax
  is   designed  and  manufactured  by
  Chautauqua Metal  Finishing  Supply  of
 Jamestown, NY. It is a modular design of
 cleaning  and rinsing  tanks, employing an
 aqueous  cleaning agent  within the ultra-
 sonic tank to accelerate and facilitate the
 cleaning action (i.e., cavitation). Miraclean
 systems  have a variety  of available op-
 tions  such as  additional  rinse  tanks and
 dryer station to meet individual customer
 needs.
  The ultrasonic cleaning system  pur-
 chased by Conax entails six cleaning sta-
 tions (see Figure 1).  At Station  1, small
 parts  were placed in metal baskets  for
 cleaning.  Baskets were required to have
 minimal mass, be made of metal, and  be
 of open construction  to limit interference
 with the free passage of both sound waves
 and cleaning fluids.  An  overhead crane
 was used  for larger,  more cumbersome
 parts.
  Station  2, the cleaning  tank,  contained
 six ultrasonic transducers mounted on the
 side of the tank. The tank also was de-
 signed with an interior grease  trap/over-
' Mention of trade names or commercial products does
 not constitute endorsement or recommendation for
 use.
  flow weir and sparger system to remove
  insoluble oils and extend bath life.
     Stations 3 and 4 are counterflow rinse
  tanks. A counterflow rinse was incorpo-
  rated to minimize fresh water  use.  The
  rinse tanks diluted the concentration  of
  cleaner that remained  on the  part after
  cleaning. The first rinse tank, Station  3,
  has an overflow weir that collects insoluble
  solution that remains on the part.
    Station 5 incorporates a final hot rinse
  into the system. Heat was added to facili-
  tate part drying subsequent to cleaning.
    Station 6 provided an area for  unload-
  ing parts from baskets. An air  gun was
  provided to facilitate  drying of parts with
  configurations that tended to retain water
  (i.e., dead end tap holes).
    Overall dimensions of the Miraclean sys-
  tem are  10' x 6.5' x 3' high. Fiberglass
  covers were installed to retain heat, con-
  serve energy, and reduce evaporation and
  humidity in  the work area.
    Samples  of the wash tank  (Station 2),
  rinse tank  (Station 4),  and final hot dip
  tank  (Station 5)  were taken  to be ana-
  lyzed for oil and grease and total organic
  carbon.  Samples were  taken  just before
  changeout of the wash tank, of the wash
  solution  after neutralization, and early in
  the use of fresh solution  to track the con-
  centration of organic contaminants  in the
  system.

  Results and Discussion

  Historical Background
   For comparison  purposes, historical in-
 formation on fugitive emissions reporting
 and hazardous waste  generation was ac-
 quired from Conax. Fugitive emission data
 was collected from Form "R" reports. To-
 tals for each are shown in Table 1.
   A significant reduction  in fugitive emis-
 sions is noted from 1987 to 1990 resulting
 from the elimination  of  bench top  freon
 cleaning units at the machining  areas. Fu-
 gitive volatile emission  reductions from the
 1990 efforts  also resulted in the  elimina-
 tion of the Blakslee freon vapor degreasing
 unit. The Miraclean system was installed
 in August 1991.
  A log of cleaning activity was kept for 2
 wk during January 1992 (1/13-24/92). En-
 gineers at Conax described this 2-wk pe-
 riod as typical of production for the facility.
 Information was gathered  on 131 batches
 of parts  cleaned during the 2-wk period.
 Average time/batch spent in the  Miraclean
 unit  is approximately 8  min. This  com-
 pared  well with the 7 min/cycle  for the
 vapor degreasers.
  Wastes associated  with  the  vapor
degreasing units included emissions and
stillbottoms estimated at 26 drums/yr and

-------
    Station    Station
      6          5
                            Station
                              4
Station
  3
Station
  2
           Station
               1
  Fresh '
Water Feed
                                                   \
                                                                \
                                                                      Parts
                                                                   \ Rinse Water
                                                                       To Drain
          Hot Rinse Tank
              180°F
                            Second
                           Counterflow
                           Rinse Tank
                           Ambient T"
   First
Counterflow
Rinse Tank
Ambient T°
Ultrasonic Clean
     Tank
   150-180°F
 Figure 1. Conax's Miraclean System Schematic.
 Table 1. Historical and Projected Emissions and Waste Generation
Year
1987
1988
1989
1990
199r
1992f
Fugitive Emissions
(Ib)
25,215
32,990
12,819
10,876
6,900
3,450
Hazardous Waste
(Ib)
2,670
1,290
4,400
1,595
1,890
1,380
 " Estimated for remainder of 1991.
 * Projected lor 1992.

 1,134,000  million gal/yr of  non-contact
 cooling water. The water-based cleaning
 medium used in the Miraclean system gen-
 erated an estimated 1050 Ib/yr of waste
 that, subsequent to  neutralization, could
 be sewered along with the 567,000 gal/yr
 of rinsewater. Approximately 55 gal/yr (450
 Ib) of oil collected by the ultrasonic clean-
 ing process was sent for fuel blending.

 Fugitive  Emission Reduction
   Emissions generated at Conax  origi-
 nated from cleaning operation at the ma-
 chining centers, the assembly tables, and
 the Blakslee vapor degreaser. The elimi-
 nation  of CFC use at the machining cen-
 ters by substituting aqueous cleaners into
 the bench  top ultrasonic  cleaning  units
 reduced emissions by 14,500 Ib/yr over a
 period from 1987 to 1990.
  The  elimination of the Blakslee vapor
degreaser further reduced emissions to a
                                          projected total of 3,450 Ib/yr for 1992, a
                                          reduction of 68% from 1990. Total volatile
                                          emission reduction projections, from 1987
                                          to 1992, are 86% from 25,215 to 3,450 Ib/
                                          yr  resulting from  the  two  operational
                                          changes.

                                          Economic Analysis
                                            An economic analysis of the changeover
                                          from CFC vapor degreasing using the
                                          Blakslee unit to  the Miraclean  ultrasonic
                                          system  utilizing an aqueous-based clean-
                                          ing solution  is included as  part  of the
                                          project.
                                            Fixed and variable costs have been con-
                                          sidered  as part  of  the evaluation. Fixed
                                          costs include the cost for equipment and
                                          installation of the Miraclean system. These
                                          costs include  the  ultrasonic equipment,
                                          NEMA  enclosure,  three tank system,
                                          pumps,  filter, sparger pump, tank covers,
                                          overhead crane,  supplies, and labor.
   Variable costs included in the economic
 assessment were  raw materials,  power
 costs, sewer fees, off-site disposal, water
 costs, and labor. Raw material cost was
 determined using 1990 cost data and ma-
 terial use  supplied by Conax. Labor cost
 was  estimated  using  $15/hr as a  basis.
 Sewer  fees and water cost  information
 was  supplied by Conax.  Total operating
 costs were determined as a summation of
 variable costs.
   A  total  operating  cost/batch of parts
 cleaned was also determined for compari-
 son.
   Based on these costs, annual savings
 and  a  payback period for the  new
 Miraclean  system were calculated for the
 project.
   The total fixed costs for the Miraclean
 system according to information provided
 by Conax  was  $44,411.  Variables costs
 calculated  for the two systems are listed
 in Table 2.
   Annual  savings projected using  the
 aqueous ultrasonic system was calculated
 to be $27,178. This resulted in a per batch
 savings  of  $7.94 ($7.26/batch  vs. $15.20/
 batch for vapor degreasing).  A payback
 period for  the system using the savings
 calculated  and  reported total costs was
 determined to be 1.6 yr.
   As the cost for the use of  CFCs con-
 tinue to  increase as  anticipated, the im-
 pact to the economics associated with the
 substitution of ultrasonic aqueous clean-
 ing would be even more favorable.

 Conclusions
   With the  installation of an ultrasonic parts
 cleaning unit utilizing  water-based clean-
 ers, the  elimination of vapor degreasing
 using solvent-based cleaners  is possible
 without  impacting cleaning quality.  A re-
 duction in the generation of fugitive  emis-
 sions and hazardous waste associated with
 a vapor  degreaser is  realized along with
 cost savings.
  The quality of the cleaning realized by
 Conax as a result of the changeover is as
 good, or in some cases, better than with
 vapor degreasing. Freon-cleaned products
 would, at times, have a slight powder resi-
 due deposition after drying. This is be-
 cause of  the inability of solvents to dissolve
 inorganic salts that accumulate  on the
 parts. No such problem was encountered
 with the  Miraclean  system. At  no time
 during the evaluation were parts returned
 for recleaning by Conax's  inhouse quality
 assurance or assembly departments.
  Freon  use was reduced by approxi-
 mately 77% (1990 to 1992). Annual waste
 reduction realized was over 12,000 Ib when
fugitive emissions are included. Transport
                                                                   &U.S. GOVERNMENT PUNTING OFFICE: MM - 5M4C7/MIM

-------
and  fate of wastes changed from  pre-
dominantly  uncontrolled air emissions of
freon to predominantly cutting and clean-
ing rinsewaters that can be sewered and
treated by the local public wastewater treat-
ment facility.

Table 2. Variable Costs
Freon Vapor
Degreaser
($)
Utility Costs
Labor Costs
Raw Material Costs
Water Costs
Sewer Costs
Off-Site Disposal
Total Operating Costs
1,559
8,205
33,939
1,780
6,200
370
52,053
  An annual cost savings of $27,178 was
calculated and results primarily from a re-
duction in raw material costs, a savings
that is anticipated to become more signifi-
cant over time. This savings  provides a
1.6 yr payback period for the project.
                                                               Aqueous Ultrasonic
                                                                 Cleaning System
                                                              	($)

                                                                    8,087
                                                                    8,295
                                                                    1,203
                                                                      890
                                                                    6,200
                                                                      200
                                                                   24,875
  The  benefits realized by Conax as a
result of the replacement  of the solvent
vapor degreaser with an ultrasonic water-
based  cleaning system  include reduced
fugitive emissions; reduced hazardous ma-
terial handling  and waste generation; and
improved cleaning efficiency, working en-
vironment, and community relations. The
results  of this  evaluation  conclude that
ultrasonic cleaning  using  water-based
cleaners provides a viable and economi-
cally advantageous alternative to the prob-
lems associated  with solvent  vapor
degreasing.
  The  full report was submitted in fulfill-
ment of CR-816762-02-0 by Erie County
Department of  Environment and Planning
under the sponsorship of the U.S. Envi-
ronmental Protection Agency.
 P. B. Kranz is with Erie County Department of Environment and Planning, Buffalo,
   NY 14202; T. Gardner-Clayson, K.C. Malinowski, T.D. Schaab, andJ.E.
   Stadelmaier are with Recra Environmental, Inc., Amherst, NY 14228; and
   Paul M. Randall (also the EPA Project Officer, see below) is with the Risk
   Reduction Engineering Laboratory, Cincinnati, OH, 45268
 The complete report, entitled "Ultrasonic Cleaning as a Replacement for a Chloro-
 fluorocarbon-BasedSystem," (Order No. PB94-121 696/AS; Cost: $27.00, subject
     to change) will be available only from:
         National Technical Information Service
         5285 Port Royal Road
         Springfield, VA 22161
         Telephone: 703-487-4650
 The EPA Project Officer can be contacted at:
         Risk Reduction Engineering Laboratory
         U.S.  Environmental Protection Agency
         Cincinnati, OH 45268
  United States
  Environmental Protection Agency
  Center for Environmental Research Information
  Cincinnati, OH 45268

  Official Business
  Penalty for Private Use
  $300
                                                       BULK RATE
                                                 POSTAGE & FEES PAID
                                                           EPA
                                                     PERMIT No. G-35
  EPA/600/SR-93/223

-------