United States Environmental Protection Agency Risk Reduction Engineering Laboratory Cincinnati, OH 45268 Research and Development EPA/600/SR-93/223 February 1994 &EPA Project Summary Ultrasonic Cleaning as a Replacement for a Chlorofluorocarbon-Based System P. B. Kranz, T. Gardner-Clayson, K. C. Malinowski, T. D. Schaab, J. E. Stadelmaier, and P. M. Randall The study summarized here evalu- ated, on a technical and economic ba- sis, the replacement of a solvent vapor degreasing system using chlorofluoro- carbons (CFC-113) with an ultrasonic cleaning system using a heated water- based cleaning fluid for cleaning stain- less steel parts. The intent of the substitution was to reduce fugitive volatile emissions while eliminating the use and handling of haz- ardous materials at the facility. The ul- trasonic cleaning system was custom fabricated to meet the dimensions re- quirements of the parts fabricated on site. Cleaning standards for the new system were to remain consistent with the criteria used for vapor degreasing. Through the utilization of an ultra- sonic cleaning system, fugitive emis- sions have been significantly curtailed. Volatile emissions are estimated to be reduced 68% (3,450 vs. 10,876 Ib/yr) over the period 1990 to 1992. This re- duction was in addition to the elimina- tion of bench top freon cleaning units at the facility, which reduced emissions from 25,215 to 10,876 Ib/yr from 1987 to 1990. The elimination of 26 drums/yr of still bottoms generated through sol- vent reclamation was also realized. To complete the economic evalua- tion, the costs of raw material (clean- ers), utilities, and labor was considered along with waste disposal. An annual savings, utilizing the ultrasonic clean- ing system, was projected to be $27,875 with the most significant savings real- ized with the cost differential in raw materials because of the high cost of chlorofluorocarbon cleaning solvents. A payback period of 1.6 yr was calcu- lated for the project. Additional benefits from the emission reduction include improved working en- vironment, reduced indoor air pollut- ants, and better community relations. This Project Summary was developed by EPA's Risk Reduction Engineering Laboratory, Cincinnati, OH, to announce key findings of the research project that is fully documented in a separate report of the same title (see Project Report ordering information at back). Introduction The use of CFCs in vapor degreasing cleaning systems has been the accepted standard in various industries for many years. This process has been universally accepted because of the efficiency and ease with which parts are cleaned and the subsequent compliance with quality control standards for cleanliness of the parts or materials cleaned. In recent years, however, the disadvantages of this tech- nology have become increasingly appar- ent — the process' generation of fugitive emissions resulting in reporting require- ments under SARA Title III, concerns about employee health and safety, and increased cost and taxation of CFCs. Furthermore, CFCs are targeted for eventual elimina- tion because of their ozone depleting char- acteristics. The project objectives were to evaluate the technical feasibility, performance, eco- nomic impact, and reduction of fugitive volatile emissions resulting from the sub- Printed on Recycled Paper ------- stitution of vapor degreasing with aque- ous ultrasonic cleaning. This is a study of the effectiveness and applicability of ultrasonic cleaning using a heated water-based cleaner as a means to clean stainless steel components. An evaluation was completed under the Erie County/EPA WRITE Program as a joint effort by Conax Buffalo Corp., Cheektowaga, NY; Erie County Environmental Compliance Services, Buffalo, NY; Recra Environmen- tal, Inc., Amherst, NY; and the U.S. Envi- ronmental Protection Agency, Office of Research and Development, Cincinnati OH. Procedure The industrial participant for this pro- gram was Conax Buffalo Corporation (Conax). Conax has been engaged in the design and manufacture of highly engi- neered, precision products for industrial, aerospace, nuclear, fiber optic, and mili- tary applications. At Conax, stainless steel, aluminum and copper parts coated with standard screw oils, water-based coolants, inhouse shop dirt, and metal shavings are cleaned in a series of cleaning and rinsing tanks of modular design using a heated alkaline solution. Previously, cleaning ac- tivities involved the use of two types of freon-based solvents that generated more than 10,000 Ib of fugitive emissions annu- ally from two vapor degreasers and two work bench stations. Since 1990, chlorinated solvents and chlorofluorocarbons (CFC-113) including trichloroethylene, 1,1,1-trichloroethane, trichlorotrifluoroethane (freon), and a freon/ acetone mixture have been used at Conax. The CFCs are used for both degreasing parts after machining, and cleaning parts prior to assembly, shipment, or stock. Un- til recently, four operations within Conax utilized chlorinated solvents and CFCs. These include machining centers parts cleaning, machine shop vapor degreasing, assembly vapor degreasing, and final as- sembly cleaning. Because of their ozone depleting char- acteristics, CFCs are targeted for even- tual elimination per the 1987 Montreal Protocol and Clean Air Act. The costs of CFCs are increasing and the use of CFCs is going to be taxed. Reclamation of CFCs generates stillbottoms that are F002 haz- ardous waste. The ultrasonic parts clean- ing system was installed to avoid and eliminate the problems associated with fur- ther CFC use. For 2 wk in January 1992, the ultra- sonic cleaning system was evaluated for 131 batches of parts ranging from large tubes to pins and from 1 to several thou- sand parts/batch. Because this was con- sidered typical production, the results would be extrapolated to an annual basis. Average cleaning times and chemical ad- dition requirements were documented, and subjective quality control inspections were done on each batch. Project forms devel- oped for the project tracked the time in minutes for each batch at each station in the cleaning process. Clean and rinse tank pH was monitored along with the clean and heated rinse tank temperatures. The number and description of parts in each batch were also listed on another project form. Averages for processing times, pH, and temperatures were calculated along with totals for a breakout of batch part quantities from 1 to 15, 15 to 100, 100 to 1000 and 1000+ parts/batch. The batches of tubes cleaned during the monitoring period were totaled. The 8- ft-long tubes were of particular interest due to the part configuration. To limit fugi- tive emissions, the surface area and work- ing area of the vapor degreasers were limited. This required a "double dip" pro- cedure for cleaning the 8-ft-long tubes. Because of the length of the tubes, this procedure required an extended period of CFC use resulting in greater emission gen- eration. The ultrasonic cleaner was de- signed to accommodate long tubes in a "single dip" cleaning operation eliminating the emissions and facilitating smoother parts cleaning operation. The Miraclean* system used by Conax is designed and manufactured by Chautauqua Metal Finishing Supply of Jamestown, NY. It is a modular design of cleaning and rinsing tanks, employing an aqueous cleaning agent within the ultra- sonic tank to accelerate and facilitate the cleaning action (i.e., cavitation). Miraclean systems have a variety of available op- tions such as additional rinse tanks and dryer station to meet individual customer needs. The ultrasonic cleaning system pur- chased by Conax entails six cleaning sta- tions (see Figure 1). At Station 1, small parts were placed in metal baskets for cleaning. Baskets were required to have minimal mass, be made of metal, and be of open construction to limit interference with the free passage of both sound waves and cleaning fluids. An overhead crane was used for larger, more cumbersome parts. Station 2, the cleaning tank, contained six ultrasonic transducers mounted on the side of the tank. The tank also was de- signed with an interior grease trap/over- ' Mention of trade names or commercial products does not constitute endorsement or recommendation for use. flow weir and sparger system to remove insoluble oils and extend bath life. Stations 3 and 4 are counterflow rinse tanks. A counterflow rinse was incorpo- rated to minimize fresh water use. The rinse tanks diluted the concentration of cleaner that remained on the part after cleaning. The first rinse tank, Station 3, has an overflow weir that collects insoluble solution that remains on the part. Station 5 incorporates a final hot rinse into the system. Heat was added to facili- tate part drying subsequent to cleaning. Station 6 provided an area for unload- ing parts from baskets. An air gun was provided to facilitate drying of parts with configurations that tended to retain water (i.e., dead end tap holes). Overall dimensions of the Miraclean sys- tem are 10' x 6.5' x 3' high. Fiberglass covers were installed to retain heat, con- serve energy, and reduce evaporation and humidity in the work area. Samples of the wash tank (Station 2), rinse tank (Station 4), and final hot dip tank (Station 5) were taken to be ana- lyzed for oil and grease and total organic carbon. Samples were taken just before changeout of the wash tank, of the wash solution after neutralization, and early in the use of fresh solution to track the con- centration of organic contaminants in the system. Results and Discussion Historical Background For comparison purposes, historical in- formation on fugitive emissions reporting and hazardous waste generation was ac- quired from Conax. Fugitive emission data was collected from Form "R" reports. To- tals for each are shown in Table 1. A significant reduction in fugitive emis- sions is noted from 1987 to 1990 resulting from the elimination of bench top freon cleaning units at the machining areas. Fu- gitive volatile emission reductions from the 1990 efforts also resulted in the elimina- tion of the Blakslee freon vapor degreasing unit. The Miraclean system was installed in August 1991. A log of cleaning activity was kept for 2 wk during January 1992 (1/13-24/92). En- gineers at Conax described this 2-wk pe- riod as typical of production for the facility. Information was gathered on 131 batches of parts cleaned during the 2-wk period. Average time/batch spent in the Miraclean unit is approximately 8 min. This com- pared well with the 7 min/cycle for the vapor degreasers. Wastes associated with the vapor degreasing units included emissions and stillbottoms estimated at 26 drums/yr and ------- Station Station 6 5 Station 4 Station 3 Station 2 Station 1 Fresh ' Water Feed \ \ Parts \ Rinse Water To Drain Hot Rinse Tank 180°F Second Counterflow Rinse Tank Ambient T" First Counterflow Rinse Tank Ambient T° Ultrasonic Clean Tank 150-180°F Figure 1. Conax's Miraclean System Schematic. Table 1. Historical and Projected Emissions and Waste Generation Year 1987 1988 1989 1990 199r 1992f Fugitive Emissions (Ib) 25,215 32,990 12,819 10,876 6,900 3,450 Hazardous Waste (Ib) 2,670 1,290 4,400 1,595 1,890 1,380 " Estimated for remainder of 1991. * Projected lor 1992. 1,134,000 million gal/yr of non-contact cooling water. The water-based cleaning medium used in the Miraclean system gen- erated an estimated 1050 Ib/yr of waste that, subsequent to neutralization, could be sewered along with the 567,000 gal/yr of rinsewater. Approximately 55 gal/yr (450 Ib) of oil collected by the ultrasonic clean- ing process was sent for fuel blending. Fugitive Emission Reduction Emissions generated at Conax origi- nated from cleaning operation at the ma- chining centers, the assembly tables, and the Blakslee vapor degreaser. The elimi- nation of CFC use at the machining cen- ters by substituting aqueous cleaners into the bench top ultrasonic cleaning units reduced emissions by 14,500 Ib/yr over a period from 1987 to 1990. The elimination of the Blakslee vapor degreaser further reduced emissions to a projected total of 3,450 Ib/yr for 1992, a reduction of 68% from 1990. Total volatile emission reduction projections, from 1987 to 1992, are 86% from 25,215 to 3,450 Ib/ yr resulting from the two operational changes. Economic Analysis An economic analysis of the changeover from CFC vapor degreasing using the Blakslee unit to the Miraclean ultrasonic system utilizing an aqueous-based clean- ing solution is included as part of the project. Fixed and variable costs have been con- sidered as part of the evaluation. Fixed costs include the cost for equipment and installation of the Miraclean system. These costs include the ultrasonic equipment, NEMA enclosure, three tank system, pumps, filter, sparger pump, tank covers, overhead crane, supplies, and labor. Variable costs included in the economic assessment were raw materials, power costs, sewer fees, off-site disposal, water costs, and labor. Raw material cost was determined using 1990 cost data and ma- terial use supplied by Conax. Labor cost was estimated using $15/hr as a basis. Sewer fees and water cost information was supplied by Conax. Total operating costs were determined as a summation of variable costs. A total operating cost/batch of parts cleaned was also determined for compari- son. Based on these costs, annual savings and a payback period for the new Miraclean system were calculated for the project. The total fixed costs for the Miraclean system according to information provided by Conax was $44,411. Variables costs calculated for the two systems are listed in Table 2. Annual savings projected using the aqueous ultrasonic system was calculated to be $27,178. This resulted in a per batch savings of $7.94 ($7.26/batch vs. $15.20/ batch for vapor degreasing). A payback period for the system using the savings calculated and reported total costs was determined to be 1.6 yr. As the cost for the use of CFCs con- tinue to increase as anticipated, the im- pact to the economics associated with the substitution of ultrasonic aqueous clean- ing would be even more favorable. Conclusions With the installation of an ultrasonic parts cleaning unit utilizing water-based clean- ers, the elimination of vapor degreasing using solvent-based cleaners is possible without impacting cleaning quality. A re- duction in the generation of fugitive emis- sions and hazardous waste associated with a vapor degreaser is realized along with cost savings. The quality of the cleaning realized by Conax as a result of the changeover is as good, or in some cases, better than with vapor degreasing. Freon-cleaned products would, at times, have a slight powder resi- due deposition after drying. This is be- cause of the inability of solvents to dissolve inorganic salts that accumulate on the parts. No such problem was encountered with the Miraclean system. At no time during the evaluation were parts returned for recleaning by Conax's inhouse quality assurance or assembly departments. Freon use was reduced by approxi- mately 77% (1990 to 1992). Annual waste reduction realized was over 12,000 Ib when fugitive emissions are included. Transport &U.S. GOVERNMENT PUNTING OFFICE: MM - 5M4C7/MIM ------- and fate of wastes changed from pre- dominantly uncontrolled air emissions of freon to predominantly cutting and clean- ing rinsewaters that can be sewered and treated by the local public wastewater treat- ment facility. Table 2. Variable Costs Freon Vapor Degreaser ($) Utility Costs Labor Costs Raw Material Costs Water Costs Sewer Costs Off-Site Disposal Total Operating Costs 1,559 8,205 33,939 1,780 6,200 370 52,053 An annual cost savings of $27,178 was calculated and results primarily from a re- duction in raw material costs, a savings that is anticipated to become more signifi- cant over time. This savings provides a 1.6 yr payback period for the project. Aqueous Ultrasonic Cleaning System ($) 8,087 8,295 1,203 890 6,200 200 24,875 The benefits realized by Conax as a result of the replacement of the solvent vapor degreaser with an ultrasonic water- based cleaning system include reduced fugitive emissions; reduced hazardous ma- terial handling and waste generation; and improved cleaning efficiency, working en- vironment, and community relations. The results of this evaluation conclude that ultrasonic cleaning using water-based cleaners provides a viable and economi- cally advantageous alternative to the prob- lems associated with solvent vapor degreasing. The full report was submitted in fulfill- ment of CR-816762-02-0 by Erie County Department of Environment and Planning under the sponsorship of the U.S. Envi- ronmental Protection Agency. P. B. Kranz is with Erie County Department of Environment and Planning, Buffalo, NY 14202; T. Gardner-Clayson, K.C. Malinowski, T.D. Schaab, andJ.E. Stadelmaier are with Recra Environmental, Inc., Amherst, NY 14228; and Paul M. Randall (also the EPA Project Officer, see below) is with the Risk Reduction Engineering Laboratory, Cincinnati, OH, 45268 The complete report, entitled "Ultrasonic Cleaning as a Replacement for a Chloro- fluorocarbon-BasedSystem," (Order No. PB94-121 696/AS; Cost: $27.00, subject to change) will be available only from: National Technical Information Service 5285 Port Royal Road Springfield, VA 22161 Telephone: 703-487-4650 The EPA Project Officer can be contacted at: Risk Reduction Engineering Laboratory U.S. Environmental Protection Agency Cincinnati, OH 45268 United States Environmental Protection Agency Center for Environmental Research Information Cincinnati, OH 45268 Official Business Penalty for Private Use $300 BULK RATE POSTAGE & FEES PAID EPA PERMIT No. G-35 EPA/600/SR-93/223 ------- |