United States Environmental Protection Agency Risk Reduction Engineering Laboratory Cincinnati, OH 45268 Research and Development EPA/600/SR-94/026 March 1994 Project Summary Onsite Solvent Recovery Arun R. Gavaskar, Robert F. Olfenbuttel, and Jody A. Jones This study evaluated the product quality, waste reduction/pollution pre- vention, and economic aspects of three technologies for onsite solvent recov- ery: atmospheric batch distillation, vacuum heat-pump distillation, and low- emission vapor degreasing. The atmo- spheric and vacuum distillation units were tested on spent methyl ethyl ke- tone and spent methylene chloride, re- spectively. Samples of spent, recycled, and virgin solvents at two industrial sites underwent physical and chemical tests to determine solvent quality. The quality of the recycled solvent was found to be acceptable for use in the specific applications. Significant waste reduction was achieved by reducing the volume of spent solvent to a few gallons of distillation residue needing disposal. The low-emission vapor degreaser is a fully enclosed alternative to conven- tional, open-top vapor degreasing. It was found to reduce air emissions by more than 99%, compared to a conven- tional vapor degreaser of the same pro- duction capacity. Compared to disposal, the atmo- spheric and vacuum distillation units reduced operating costs significantly. The estimated payback period for these units was found to be less than 2 yr. The low-emission vapor degreaser re- duced operating costs by reducing sol- vent losses and labor costs. The estimated payback for this unit was approximately 10 yr. The cost estimates were based on a full range of consider- ations including equipment, engineer- ing, installation, operation, mainte- nance, and energy use. The estimates did riot, however, include potential changes in liabilities or impacts due to regulations planned or in the process of being implemented. This Project Summary was developed by EPA's Risk Reduction Engineering Laboratory, Cincinnati, OH, to announce key findings of the research project that is fully documented in a separate report of the same title (see Project Report ordering information at back). introduction This; study, performed under the U.S. Environmental Protection Agency's (EPA's) Waste Reduction and Innovative Technol- ogy Evaluation (WRITE) Program, was a cooperative effort between EPA's Risk Reduction Engineering Laboratory (RREL) and the Washington Department of Ecol- ogy. The objective of the WRITE Program is to evaluate, in a typical workplace envi- ronment, examples of prototype or inno- vative .commercial technologies that have potential for source reduction or recycling. The study evaluated three technologies for recovering and reusing waste solvent on site: atmospheric batch distillation, vacuum heat-pump distillation, and low- emission vapor degreasing. Comparing the three units was not an objective of this study. Rather, the suitability of each tech- nology, to its respective application was examined. In each technology category, a specific unit offered by a specific manu- facturer was tested. Other variations of these units (with varying capabilities) may be available from several vendors. Printed on Recycled Paper ------- The two liquid-distillation units were tested at industrial sites that have pur- chased and are using the units. The at- mospheric unit was tested on spent methyl ethyl ketone (MEK) at a site where MEK is used to clean the spray painting lines between colors. The recycled solvent was reused for the same purpose, with the residue shipped off as hazardous waste. The vacuum unit was tested on spent methylene chloride (MC) at a site that manufactures wires and cables. The MC is used for cold (immersion) cleaning of wires and cables to remove markings (ink). Atmospheric Batch Distillation and Vacuum Heat-Pump Distilla- tion Atmospheric distillation is the simplest technology available to recover liquid spent solvents. Units that can distill as little as 5 gal or as much as 55 gal/batch are avail- able. Some units can be modified to oper- ate under vacuum for higher-boiling solvents (>135°C). Contaminant compo- nents with lower boiling points than the solvent or that form an azeotrope with the solvent cannot be separated (without frac- tionation) and may end up in the distillate. The unit used in this study (Figure 1) was Model LS-55D,* manufactured by Finish Thompson, Inc. The distillation residue, often a relatively small fraction of the spent solvent, is disposed of as hazardous waste. The vacuum unit tested, Model 040 is manufactured by Mentec AG in Switzer- land and supplied in the United States by Vaco-Solv Chicago, Inc. It is configured similar to a conventional vacuum distilla- tion system except that the pump, in addi- tion to drawing a vacuum, functions as a heat pump (Figure 2). No external heating or cooling is applied. The heat pump gen- erates a vacuum for distillation and com- presses vapors for condensation. Model 040 is suitable for solvents with boiling points up to 80°C, Spent solvent is con- tinuously sucked into the evaporator by a valve. The vacuum drawn generates va- pors, which are sucked into the heat pump, compressed, and sent to the condenser. The temperature stabilizes automatically according to the specific solvent and the ambient air. The condenser surrounds the evaporator to allow heat exchange be- tween the cool spent solvent and the warm condensing vapors. The product quality objective for the two liquid-distillation units was to show that the recycled solvent was of sufficient quality for reuse. One 55-gal drum of spent solvent was processed each day through the batch and continuous units. For each unit, one drum of spent solvent was pro- ' Mention ol trade names or commercial products does not constitute endorsement or recommendation for use. Contaminated Solvent Stillbag Heated Walls Electric Heat Source Reclaimed Solvent Figure 1. Atmospheric distillation unit. (Source: Finish Thompson, Inc.) cessed in ~12 hr. The atmospheric unit left 16 gal of residue and the vacuum unit left 3 gal. The amount of residue left be- hind is a function;of the application and not the distillation; units. „Samples of the spent and recycled solvents were ana- lyzed by standard ASTM method.s'tb de- termine the improvement in quality. Virgin solvent samples also were collected at each site and subjected to the same tests for comparison. : During the vacuum unit test, the "virgin" sample was found to be a sample of MC obtained by the site from a solvent recy- cling company. Th,e "virgin" solvent speci- fications meet the requirements for the company's application, and it has been used satisfactorily at the site in the past. The vacuum unit was being operated at a faster rate than. recommended by the manufacturer. Bebause the unit's built-in condenser-evaporator heat exchange was not sufficient for this rate, site personnel had attached an lair-cooled condenser at the outlet to restrict vapor loss to -4 gal/ 55 gal of spent solvent. To prevent the release of this vapor into the work area, the vapor was led through a pipe to the roof of the facility and discharged per state regulations. Table 1 shows the characterization re- sults for samples from the atmospheric and vacuum units. In appearance and color, the spent samples varied vastly from the clear recycled and virgin samples. All the measured parameters showed a sig- nificant improvement from spent to re- cycled samples but were not quite up to virgin grade. The water content increase in the recycled samples from the atmo- spheric unit was traced to a slight leakage from the water-cooled condenser that was worn out due to long use. Repairing the leak after the testing, site personnel re- ported that the problem had been cor- rected. : MEK purity of the recycled sample from the atmospheric unit substantially in- creased from 78% to -85%. The large decrease in nonvolatile matter during re- cycling accountsifor most of this increase. Of the 15% impurity in the recycled sample, 5% is water as discussed above. The remaining 10% impurity probably is due to the codistilling out of paint thinner solvents (proprietary blends) present in the spent solvent. MC purity of the re- cycled solvent from the vacuum unit was 86%, comparing lavorably with the "virgin" sample purity of [90%. Some performance characteristics of MC (a halogenated solvent) also were evalu- ated. The pH of the water extract of the recycled solvent was fairly close to the "virgin" value of; 7. The spent sample pH ------- Condensate Trap Vapor Filter Overflow Protection *- Feed Level Control Spent Solvent Vaporizer Residue Slu Condenser Distillate Figure 2. Vacuum heat-pump distillation unit. (Source: Vaco-Solv Chicago, Inc.) of 5 indicates the presence of potentially corrosive components. The corrosion test on steel and aluminum (ASTM D2251) yielded noticeable corrosion only in the case of the steel strip placed in the spent solvent sample. No such corrosion was evident due to the recycled solvent, indi- cating that recycling improved the quality. Table 2 shows the waste reduction achieved by the two distillation technolo- gies at the respective sites. Through recy- cling, large volumes of spent solvent waste were reduced to small volumes of distilla- tion residue, which is disposed of as RCRA hazardous waste. Both MEK and MC are hazardous chemicals listed on the Toxic Releases Inventory (TRI). These solvents also are on EPA's list of 17 chemicals targeted" for 33% reduction by 1992 and 50% reduction by 1995. The economic evaluation compares the costs of each new technology to conven- tional practice. Table 3 shows the major operating costs associated with disposal and the atmospheric batch unit. For the unit, recycling saved ~$10,000/yr. The pur- chase price of the atmospheric batch unit is $12,995. A detailed calculation based on worksheets provided in the Facility Pol- lution Prevention Guide (EPA, 1992) indi- cated a payback period of less than 2 yr. For the vacuum unit (Table 4), savings from recycling are ~$18,300/yr. An explo- sion-proof vacuum unit costs $23,500. The payback period for this unit also was less thsin 2 yr. Low-Emission Vapor Degreasing (LEVD) LEVD currently is used in Europe, where vapor degreasers are regulated as a point source. Previous studies (Battelle, 1992) on conventional open-top vapor degreas- ers have shown that a large part of the solvent (more than 90% in some cases) is losit through air emissions, which are con- siderable even though vapor degreasers are required to have primary cooling coils (ta.pwater cooled) and a certain freeboard height. Air emissions are mainly workload- related, caused either by dragout of sol- vent on the workload itself (and subsequent vaporization) or by disturbance in the air-vapor interface during entry and Table 1. Characterization of Solvent Samples Sample Appearance Atmospheric Unit (MEK) Spent Dark grey w/sediment Recycled Clear Recycled Dupd Virgin Vacuum Unit (M( Spent Recycled Recycled Dupd Virgin Clear Clear y ' : Dirty grey-brown Clear Clear Clear, tinge of yellow Color3 __Q 5 5 5 a 5 5 10 Specific Gravity 0.845 6.827 0.821 0.800 1.220 1.286 1.288 1.298 Nonvolatile Matter mg/100mL 6,951 2.6 2.0 2.2 34,101 20.37 17.88 57.16 Conductivity /j,mhos/cm 7.05 3.30 3.40 1.15 1,063 137 136 36 Water Content i %bywt 1.89 5.42 5.56 .0.09 0-27 : 0.25 ! 0.24 0.14 Acid Acceptance*1 NA< , NA NA . ' ' NA- ..'--. • . , 0.032 0.004 0.005 0.003 " Purity %c 78.41 • 85.02 85.54 99.09 NA' 86.4 NA 90.1 aOna scale of 5 to 500, with 500 being the darkest color. ASTM D1209 and D2108. h Measured as equivalent NaOH wt%. ASTM D2942. c Gas chromatography analysis based on ASTM D2804. d Duplicate analysis of the same sample. e Not comparable with standards. Sample was too dirty. • ' NA = not analyzed. ------- Table 2. Waste Reduction by Atmospheric and Vacuum Units -Disposal Option - Wastestream Annual Volume - Recycling Option - Wastestream Annual Volume Atmospheric Un'rt'Test Site: Spent MEK Drums Vacuum Unit Test Site: Spent MO Drums 880 gal 17 drums 3,000 gal 55 drums Distillation residue Still bags Cooling water Drums Distillation residue Air emission Drums Used oil 262 gal 17 bags ,18,360 gal 5 drums 136 gal 218 gal 3 drums 1gal Table 3. Major Operating Costs for Atmospheric Unit Item Disposal Option Virgin solvent Disposal -labor — drums — disposal fee Atmospheric Unit Virgin solvent Operating labor Routine maintenance -spare parts -labor Energy Cooling water Disposal -labor -drums —residua disposal —still bags Annual Usage 880 gal 8hr 17 900 gal 245 gal 17hr 1 12hr 1,265kWh 18,360 gal 3 5 262 gal 17 Unit Cost ($) 10.50/gal 8/hr 40/drum 400/55 gal Total 10.50/gal 8/hr 86/each 8/hr 0.04/kWh ' , 1/1000 gal 8/hr 40/drum 675/55 gal 84/12 bags Total Annual Cost ($) 9,240 64 680 6.545 16,529 2,573 136 86 96 51 18 24 200 3,215 119 6,518 exit of the workload. Other sources are convection and diffusion during startup, operation, idling, shutdown, and, to a small extent, equipment leaks. Air emissions are a concern for metal finishers because many solvents used in vapor degreasing have been targeted by EPA in the 33/50 Program. Environmental and Occupational Safety and Health Administration (OSHA) regulations have become more stringent. Pollution control devices available for conventional vapor degreasers include in- creased freeboard height, refrigerated coils, and covers to eliminate drafts and reduce diffusion. In contrast, LEVDs are completely enclosed, airtight units. This evatuatbn used Model 83S (Size 1), manu- factured in the United States by Durr Au- tomation, Inc. Figure 3 shows its opera- tion. About 1 hr before the shift begins, a timer switches on the heat to the sump. When the solvent in the sump reaches vapor temperature, the vapor is still con- fined to the enclosed jacket around the working chamber. The parts to be cleaned (workload) are placed in a galvanized bas- ket and lowered into the working cham- ber. Loads can range from 330 to 110 Ib (of steel parts) in this model. When the lid is shut and the unit is switched on, com- pressed air hermetically seals the lid shut for the duration of the cycle. Table 5 shows typical cleaning cycle stages. During "vapor fill," solvent vapors enter the chamber from the outer jacket, and degreasing begins. During "conden- sation," solvent vapors are condensed out by a refrigerated copling coil at the bottom of the chamber. During "air recirculation," the air-solvent mixture is recirculated through a chiller tp condense out more solvent. During "carbon heatup," solvent adsorbed in the previous cycle is released (desorbed) to the circulating air and con- denses out in the chiller. During "adsorp- tion," the chamber air is recirculated in the reverse direction-first through the chiller and then through -the carbon. Most re- sidual solvent vapor in the cold air is ad- sorbed on the carbon. A photoionizatibn detector (PID) probe verifies that the cham- ber air has less than 1 g/m3 of solvent and signals the air compressor to release the seal on the lid 'to end the cycle. If the chamber air has more than 1 g/m3 of solvent, the cycle loops back to the des- orption stage. The entire cycle is pro- grammed and requires no operator attention except to; load and unload the workload. Only a very small amount of solvent exhausts at the end when the lid is opened. The LEVD also works as a distillation unit to clean the liquid solvent in the sump. During distillation, the unit is switched on without any workload in the chamber. Testing was conducted on the LEVD using perchloroethylene (PCE) solvent. Test runs were conducted on machined steel parts with and without cutting oil on the parts. Total cycle limes were recorded for all completed runs. Because the same batch of parts was used for each run, parts were either pold (ambient) or hot depending on the cooling time between runs. Adding oil to the parts d.id not greatly affect the total cycle time, but the work- load mass did. In all the runs starting with parts dipped in cutting oil, the cleaned parts were visually examined for traces of oil or dirt contamination. No contamina- tion was noticed oni the parts from any pf these runs. ' The ppllution prevention aspect of the LEVD was the main focus of this technol- ogy. The completely enclosed design of the working chamber allows the potential for air emissions only when the cleaning cycle is complete and the lid is opened. Any solvent vapor riot evacuated from the chamber during condensation or adsorp- tion releases to the atmosphere. Table 6 shows the total cycle times and emissions recorded from the LEVD by a flame ionization detector (FID) probe in- serted (for this test) into the working cham- ber below the designated vapor level. FID measurements began during the adsorp- tion stage and continued until after the lid was opened. A second FID probe (ambi- ------- Table 4, Major Operating Costs for Vacuum Unit Item Disposal Potion Virgin solvent Disposal - labor - drums - disposal fee Virgin solvent Operating labor Energy Disposal - still bottoms — used oil -labor - drums Routine Maintenance -oil - spare parts - labor Annual Usage 3000 gal 16 hr 55 3000 gal 246 gal 55hr 985 kWh 136 gal 4 quarts 3hr '3 4 quarts a 16 hr Unit Cost ($) 3.57/gal 8/hr 40 2.50/gal Total 3.57/gal 8/hr 0.04/kWh 2.50 3.00/quart 8/hr 40/drum 3.50/quart 480 (max)3 8/hr Total Annual Cost ($) 10,710 128 2,200 7.500 20,538 878 220 39 340 12 24 120 14 480 128 2,255 The $480 cost for spare parts is a maximum, which assumes that the manufacturer's recommend- ations are exactly followed and that the maximum number of parts will be replaced during each overhaul. Actual maintenance costs could be lower. Working Chamber Workload Vapor Inducer Electric -» Heat Cooling Coils Li1uid Solvent Water Separator Water Liquid Solvent Legend — — — ^- Desorption Stage __ >> Adsorption Stage ^- Liquid Solvent Figure 3. Low-emission vapor degreaser. (Source: Durr Automation, Inc.) ent), positioned outside the unit near the lid seal, took continuous measurements . all around the unit during operation, with special emphasis around the lid to ensure leak-proof design. Ambient levels (3 to 4 ppm) in the indoor facility on the test days were consistent. Figure 4 shows how a typical LEVD cleaning cycle ends. The same pattern was evident in the other runs. Time zero corresponds to the start of measurements when the FID probe in the working pham- ber was activated. Just before the adsorption cycle ended, the chamber FID read 52 ppm, well below the targeted 1 g/m3 (150 ppm of PCE). When the lid was retracted, the chamber air had full access to the ambient. At this point, the chamber concentration dropped shairply as the residual solvent vapor in the chamber dispersed. The ambient FID probe showed a corresponding increase (to 6 ppm). Both FID readings soon stabi- lized to facility ambient levels (3 to 4 ppm). Later, as the basket of cleaned parts was raised out of the chamber, the sec- ond FID probe was thrust into the basket near the parts. No elevated readings above ambient were sensed, indicating that the parts were free of solvent. Thus, there is a very small air emission from the LEVD when the lid is opened. In all the test runs, the solvent concentration was well below the targeted 1 g/m3 (150 ppm PCE), so 1 g/m3 is an achievable concentration. The volume of the working chamber is 0.6 m3. Assuming that all the residual solvent vapor (1 g/m3 maximum) in the chamber is discharged. to the ambient area, the typical air emission through the opened topi is 0.6 g (0.00132 lb)/cycle or less. It takes 1 hr to clean 560 Ib of oiled steel parts. Therefore, the air emission from this LEVD mode is 0.00132 Ib of solvent/ hr. A typical conventional open-top vapor degreaser cleaning at a similar rate (~ 560 Ib of steel parts/hr) typically would emit 0.147 Ib of solvent/ft2/hr (EPA, 1989), or 0.662 Ib of solvent/hr from its 4.5-ft2 opening during continuous operation. Therefore, the LEVD reduces air emis- sions by more-than 99% compared to air emissions from the typical conventional open-top vapor degreaser (i.e., with a 0.75 fre>eboard ratio, primary cooling coil, elec- tric hoist, and no lip exhausts) used in this calculation. The OSHA exposure limit for PCE is 25 ppim for an 8-hr time-weighted average (TWA). Personnel air sampling (in accor- dsince with OSHA guidelines) was not con- ducted during this evaluation, but PCE levels measured with the ambient FID at all times during operation (3 to 4 ppm) ------- TabioS. LEVD Cleaning Cycle Stage Solvent heatup (once a day) Solvent spray (optional) Vapor fill Degreaslng Condensation Airreclrculation Carbon heatup Desorptlon Adsorption Vendor-Recommended Time Settings (sec) Variable a 10-180 Variable" 20-180 120 120 Variable0 60 60-240 " Times Set for This Testing (sec) Variable a not used Variable b 60 120 120 Variable c 60 240 • Requires ~1 hron days following overnight shutdown when sump solvent temperature drops to 70°C. After weekend shutdowns, when sump solvent temperature drops to 20°C, it may take 1.5hr for solvent to reach vapor temperature. Timer on unit allows automatic heatup. 6 Depending on the workload mass and type of metal. Varied from 8.5 mm lor 165 Ib to 36.5 mm for 915 Ib of steel parts. c Carbon heatup took approximately 22.5 min during testing. rf At 60 sec, if monitor shows that chamber concentration is above 1 g/m3, then the adsorption stage proceeds to the ful!240-sec stage. This sequence repeats if necessary. Table 6. Emissions from LEVD Run No* 1 2 3 5 6 8 Target d Mass of Steel Parts (Ib) 165 165 900 165 e 165e 915 e 560 Final Chamber Concentration11 (ppm) 52 75 92 43 47 78 150 Total PCE Emission0 (Ib/cycle) 0.0005 0.0007 0.0008 0.0004 0.0004 0.0007 0.0013 Total Cycle Time (min) 39' 67.5 50.5 40' 69 609 Emission Rate (Ib/hr) 0.0011 0.0007 0.0005 0.0006 0.0006 0.0013 Runs 4, 7, and 9 were interrupted to allow other measurements. ° At the moment when the seal on the lid is released. 0 Based on 150 ppm - 1 g/m3 of PCE and a chamber volume of 0.6 m3. ° Normally the machine is programmed to release the lid when solvent concentration in the chamber falls below 1 g/m3 (150 ppm of PCE). This target was easily met in all the test runs. 0 Workload parts were dipped in cutting oil before the run. 1 Workload parts were already hot from being used in previous runs when inserted into working chamber. Wence, total cycle times for these runs are lower than normally expected. o Expected cycle time for 560 Ib of steel parts (workload). and at the edge of the chamber opening for about 2.5 min when the lid is retracted completely (<6 ppm) (Figure 4) are well under the OSHA exposure limit. The pol- lution prevention potential of this unit is further enhanced by its ability to perform as a liquid solvent distillation system for cleaning the sump solvent; this capability was not a part of this evaluation. When pollution prevention is an objective, the LEVD also affords greater production flex- ibility because it has none of the idling losses between loads or downtime losses during shutdown of the conventional de- greaser. Table 7 lists the LEVD's major operat- ing costs and the operating costs for a conventional open-top vapor degreaser with similar production capacity. With a vendor-quoted purchase price for the LEVD of $210,000, the unit results in sav- ings in annual total operating costs of ~$25,000 mainly from reduced labor costs (due to larger batch size) and lower sol- vent requirement (due to solvent recov- ery). The LEVD pays for itself in -10 yr. The above is a straightforward cost com- parison between the LEVD and a conven- tional vapor degreaser of similar production capacity. Other cost-benefit factors must be taken into account when making eco- nomic decisions. The LEVD does not re- quire capital and operating expenditures for auxiliary equip.ment that may be re- quired for a standard conventional vapor degreaser (increased freeboard ratio, re- frigerated coils, lip exhausts, room venti- lation) in order'meet or anticipate increasingly stringent environmental and worker safety regulations. The LEVD is a self-contained unitthat requires no addi- tional facility modifications to achieve sig- nificant emission reductions. Another consideration is the LEVD's pro- duction rate. The above calculation used a production rate of 560 Ib/hr of steel parts (workload) because most vendors of conventional degreasers quote capacities based on steel parts. However, produc- tion capacity per machine can vary de- pending on the metal processed. Based on the thermal diffusivity of various met- als, total cycle times versus production rates are plotted jn Figure 5. Brass and copper can be processed faster than steel with the LEVD, and aluminum can be pro- cessed faster up to a point determined, for a certain shape of parts, by the maxi- mum mass of aluminum parts that fit into the basket. The shape of the parts also may affect cycle time. Parts with recesses that can trap solvent should be arranged in the basket so that the solvent liquid drains out. Other features offered by the vendor (oscillating or rotating baskets) should be used. Otherwise, either the air recircula- tion stage time must be increased, or the unit will loop into several adsorption cycles until the chamber concentration falls be- low 1 g/m3. Conclusions and Discussion All three technologies evaluated in this study demonstrated good potential for pol- lution prevention/waste reduction. The two onsite solvent distillation technologies re- duced large volumes of hazardous sol- vent to a few gallons of distillation residue and produced a reusable recycled prod- uct. The total U.S. solvent demand is ap- proximately 160 billion gal/yr. Therefore, there is considerable potential for recy- cling and reusing spent solvent. Between onsite" and offsite recovery, onsite recov- ery is preferable because of the reduced transportation hazard. The largest single use for solvents in the United States is for vapor degreasing. The LEVD reduced air emissions signifi- cantly compared to :emissiohs from a con- ventional vapor degreaser. Payback periods for both distillation technologies are less than 2 yr. The LEVD is a slightly higher capital investment (with ------- 10000 I f I I p 1000 100 : a payback period oi approximately 10 yr), but it eliminates the need for other poten- tially expensive auxiliary equipment that conventional vapor degreasers would re- quire to meet comparable pollution pre- vention objectives. The full report was submitted in partial fulfillment of Contract Number 68-CO-0003, Work Assignment 2-36, by Battelle under the sponsorship of the U.S. Environmen- tal iProtection Agency. 100 200 300 Time (seconds) Figure 4. Concentrations at the end of the cleaning cycle for Run 1. 400 500 600 Table 7. Operating Costs for Low-Emission Vapor Degreasing- Item Annual Volume Unit Cost ($) Total Cost ($) Conventional Degreaser Operating labor Electricity Cooling water Maintenance -labor -materials Net solvent loss 4,000 hr 25,500 kWh 480,000 gal 22 hr 2,642lb 8/hr 0.04/kWh 1/1000 gal 8/hr 0.71/Ib 32,000 1,020 480 176 $88 Total 35,640 LEVD Operating labor Electricity Maintenance - labor - materials 333 hr 93,725 kWh 262.5 hr — 8/hr 0.04/kWh 8/hr — Total 2,664 3,749 2,100 2.100 10,613 •&V.S. GOVERNMENT PRINTING OFFICE: 1994 - 550467/80201 ------- 200 400 600 SOO Mass of Parts Cleaned Per Cycle, Ib Figure 5. Variation ofLEVD cycle time for various metals. 1000 1200 Arun R. Gavaskar, Robert F. Olfenbuttel, and Jody A. Jones are with Batelle, Columbus, OH 43201. Ivars Lids is the EPA Project Officer (see below). The complete report, entitled "Onsite Solvent Recovery," (Order No. PB94- 144508; Cost: $19.50, subject to change) will be available only from National Technical Information Service 5285 Port Royal Road Springfield, VA22161 Telephone: 703-487-4650 The EPA Project Officer can be contacted at Risk Reduction Engineering Laboratory U.S. Environmental Protection Agency Cincinnati, OH 45268 United States Environmental Protection Agency Center for Environmental Research Information Cincinnati, OH 45268 Official Business Penalty for Private Use $300 BULK RATE POSTAGE & FEES PAID EPA PERMIT No. G-35 EPA/600/SR-94/026 ------- |