United States
                Environmental Protection
                Agency
 Risk Reduction
 Engineering Laboratory
 Cincinnati, OH 45268
                Research and Development
EPA/600/SR-94/074    May 1994
EPA       Project Summary
                Substituting  Cadmium  Cyanide
                Electroplating with  Zinc Chloride
                Electroplating
                B.C. Kim, P.R. Webb, J.A. Gurklis, and R.K. Smith
                 The environmental and economic im-
                plications of substituting zinc chloride
                electroplating for  cadmium  cyanide
                electroplating were evaluated. The pro-
                cess substitution successfully achieved
                product quality to satisfy the customer
                requirements for corrosion resistance.
                Corrosion resistance was determined
                by salt-spray tests in accordance with
                the  ASTM Method  B117-90. Not only
                did the process substitution eliminate
                cadmium and cyanide from the wastes
                and chlorine from the wastewater treat-
                ment process, thereby greatly reduc-
                ing  hazards  to plant personnel and
                pollution of the environment, the pro-
                cess substitution also reduced oil and
                grease waste. On the negative side,
                however, the process change increased
                the  generation of wastewater, waste-
                water treatment sludge, and chromium.
                For a new installation, the zinc-plating
                process offers an economic advantage
                of slightly lower operation cost over
                the cadmium-plating process.
                  This Project Summary was developed
                by EPA's Risk Reduction Engineering
                Laboratory, Cincinnati, OH, to announce
                key findings of the research project
                that is fully documented in a separate
                report of the same title (see Project
                Report ordering information at back).

                Introduction
                 This study, performed under the U.S.
                Environmental Protection Agency's (EPA's)
                Waste Reduction Innovative Technology
                Evaluation (WRITE) Program, was a co-
                operative effort between EPA's Risk Re-
                duction Engineering  Laboratory (RREL)
and Aeroquip Corporation. The objective
of the WRITE program is to evaluate, in a
typical workplace environment, examples
of prototype technologies that have po-
tential for reducing wastes. Substitution of
zinc chloride electroplating  for cadmium
cyanide electroplating was  evaluated at
Aeroquip's Industrial Connectors Division*
in Van Wert, OH. The goal of this project
was to evaluate (1) the effects of the pro-
cess substitution on  product quality, (2)
the waste reduction/pollutant reduction ef-
fects of the process substitution, and (3)
the economics of the process substitution.

The Processes
  The cadmium cyanide and the zinc chlo-
ride plating processes for the rack plating
line at Aeroquip are compared in Table 1.
Hydrochloric acid is used to condition parts
(shown  as step 12  in  Table 1) before
plating  in the zinc chloride  process
whereas sodium cyanide is used in the
cadmium cyanide process. The cadmium
cyanide plating line had separate tanks to
apply either clear chromate or yellow chro-
mate coatings (steps 18 and 20 in Table
1). Previously, Aeroquip used clear chro-
mate coating on most (90% to 95%) of
the  cadmium-plated parts. Currently,
Aeroquip uses yellow chromate coating
on all zinc-plated  parts because (1)
Aeroquip has adopted a worldwide stan-
dardization of yellow as the color for their
fittings and (2) yellow chromate coating
vastly improves the corrosion protection
* Mention of trade names or commercial products does
 not constitute endorsement or recommendation for
 use.
                                                                 Printed on Recycled Paper

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Tab/a 1. Comparison of Zinc Chloride and Cadmium Cyanide Back Plating Processes

                                                   Operation
Process
Step
1
2
3
4
5
6
7
8
9
10
11
12
13
14
15
16
17
18
19
20
21
22
Tank
No.
1
2
3
4
5
6
7
8
9
10
11
12
13
14
15
16
17
18
19
20
21
'22
Zinc Chloride
Plating Line
Soak clean
Rinse
Electroclean
Rinse
Rinse
Hydrochloric acid pickle
Rinse
Rinse
Electroclean
Rinse
Rinse
Hydrochloric acidpre-dip
Zinc plating
Rinse
Rinse
Nitric acid dip
Yellow chromate dip
Rinse
Chromate seal
Rinse
Drip tank dip
Water-soluble oil dip
Cadmium Cyanide
Plating Line
Soak clean
Rinse
Electroclean
Rinse
Rinse
Hydrochloric acid pickle
Rinse
Rinse
Electroclean
Rinse
Rinse
Sodium cyanide pre-dip
Cadmium plating
Rinse
Rinse
Rinse
Nitric acid dip
Clear chromate dip
Rinse
Yellow chromate dip
Rinse
Water-soluble oil dip
of the zinc-plated fittings. The yellow chro-
mate solution used by Aeroquip contained
approximately a five times greater chro-
mium concentration than did the clear chro-
mate solution. In the  water-soluble oil
application step (step 22 in Table  1), the
concentration of the oil was reduced  by a
factor of approximately ten  in the  zinc
chloride plating process from the level used
In the cadmium cyanide plating process.
The change was necessary to obtain im-
proved adhesion of chromate coating dur-
ing the subsequent heat-curing step.
   Rinse water and various cleaning and
plating solutions are discharged continu-
ously  or periodically dumped from the
tanks and treated in an on-site wastewa-
ter treatment  plant.  All wastes from the
plating operations eventually are in three
waste streams — treated wastewater, de-
watered sludge, and waste oil — that are
discharged or disposed from the  waste-
water treatment plant. The treated  waste-
water is discharged to  a  sanitary  sewer.
The dewatered sludge is collected  in a
20-yd3 hopper and sent to an off-site haz-
ardous landfill once a month. The waste
oil Is collected in drums  and sent to an
off-site hazardous waste incinerator every
3 mo.

 Product Quality Evaluation
   Product quality was  measured  by the
corrosion resistance of plated parts deter-
 mined by salt-spray (fog) tests carried out
In accordance  with  the  ASTM  Method
 B117-90 (Standard Test  Method  of Salt
Spray [Fog] Testing). As part of their qual-
ity acceptance criteria for zinc-plated parts,
Aeroquip's engineering process specifica-
tion has adopted the ASTM Method B633-
85 (Standard Specification  for  Electro-
deposited Coatings of Zinc on Iron and
Steel)  requirement of 96  hr  of freedom
from white corrosion products in salt-spray
testing. Most Aeroquip customers require
96 hr before the first appearance of white
corrosion on zinc-plated parts. The pro-
cess specification for some of Aeroquip's
products has an additional  internal accep-
tance  criterion  (not required  by custom-
ers) of 360  hr  of exposure to salt spray
before the first appearance of red rust.
   In the first series of tests, four repre-
sentative types of parts plated with zinc in
the rack plating line were tested in parallel
by Aeroquip  and  an independent testing
laboratory (Detroit Testing Laboratory, Inc.
[DTL],  Warren, Ml). These parts, shown in
Figure 1, included swivel  nut (Group B)
and three types of adapter (Groups A, C,
and D). In the DTL tests, all of the Group
A, B, and D specimens were free of white
corrosion products at  120 hr, so that the
96-hr  requirement of  no white corrosion
for zinc-plated parts was met. Very slight
white corrosion was noted on some Group
C specimens at 120 hr. In the DTL tests,
all specimens in Groups A, B, and D were
free of red rust at the end of the 360-hr
observation period; two of the six speci-
mens  in Group C showed red rust at the
336-hr and 360-hr observation periods. In
the Aeroquip tests, there was no sign of
 white  corrosion products on any of the
 specimens in any of the groups at the 96-
 hr observation  period. Further, the ex-
 tended-exposure tests showed that only
 one of six specimens in Group D exhib-
 ited red rust at 264 hr. Thus, of a total 24
 specimens tested by Aeroquip, only one
 specimen definitely would not have met
 Aeroquip's  internal requirement of  free-
 dom from red rust at 360 hr. One speci-
 men in Group B exhibited!red rust at 408
 hr; at  336 hr, no specimens in this group
 showed red rust. In  general,  very  good
 agreement  and full  compliance with the
 requirement for absence of white corro-
 sion products for 96 hr was noted for the
 groups of specimens tested at both labo-
 ratories. Further, there was generally good
 agreement  in results with  respect to the
 appearance of red rust. At both laborato-
 ries, only 3 of 48 specimens did not meet
 the Aeroquip's internal requirement of free-
 dom from red rust for 360 hr of exposure
 to salt-spray.
   Aeroquip also tested four groups of parts
 platedjwith  zinc in the barrel plating lines.
 The parts included nipple (Group A),  crimp
 socket (Group B), and two other types of
 socket (Groups C and D). All specimens
 in all  four groups met the requirement of
 freedom from white corrosion products at
 96  hr. White corrosion started to appear
 on  most of the specimens at the 168-hr
 observation point. All parts also  met the
 requirement of no red rust at 360 hr. One
 specimen in Group A exhibited red rust at
 432 hr. At 504 hr, red rust was present on
 Group A and Group C parts, but Group B
 and Group D specimens showed no red
 rust.
   From October 15 to  November  5,
 1991, Aeroquip  carried  out  corrosion
 tests  to compare the salt-spray corro-
 sion resistance of zinc-plated parts with
 cadmium-plated parts. Seven groups of
 representative parts plated with zinc and
" seven groups  of identical parts plated
 with  cadmium were tested. The parts
 included two types  of barrel-plated reus-
 able sockets (Groups A and B), two types
 of barrel-plated reusable nipples (Groups
 C and D),  two types of rack  plated nuts
 (Groups E and F), and a rack-plated crimp
 fitting (Group G). The results of the salt-
 spray tests on the zinc-plated parts were
 as  follows: (1) all specimens in the  seven
 groups of parts passed the requirement of
 96 hr before the first appearance of white
 corrosion  products;  (2) no red  rust ap-
 peared on any of the specimens  in the
 seven groups at the 360-hr observation
 time; (3) all specimens in Groups A, B, D,
 and G were still free of red rust after 504
 hr  of salt-spray exposure; red rust was

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Group A: Part No. 2021-2-35; Pipe to 37 ° mate Hare adapter
Group B: Part No. 210204-12s; swivel nut (crimp type)
Group C: Part No. 206204-8-6s; SAE male to 37' male flare adapter
Group D: Part No. 2089-6-6s; 90 ° male to female pipe adapter

Figure 1. Zinc-plated parts salt-spray tested by Detroit Testing Laboratory andAeroquip (rack plated).
beginning to  develop on  specimens in
Groups C, E, and F at 504 hr. The results
of the salt-spray tests on cadmium-plated
parts were as follows: (1) all specimens in
the seven groups passed the requirement
of 96 hr before the  first appearance of
white corrosion products, and the appear-
ance of white corrosion products in any of
the seven groups was delayed to 336 hr
and beyond and (2) no red rust was ob-
served  on any of the  cadmium-plated
specimens after 504 hr of exposure, at
which point the tests  were ended. These
results  demonstrated that  the  cadmium-
plated parts exhibit superior corrosion re-
sistance to zinc-plated parts with regard
to the appearance of white corrosion prod-
ucts and red  rust in salt-spray tests.

Waste Reduction Potential
   Waste reduction potential of the pro-
cess substitution was determined on the
basis of waste volume reduction and pol-
lutant reduction. Waste volume reduction
was estimated for the treated wastewater
and the dewatered sludge,  which, respec-
tively, affect  conservation  of water and
landfill space. Pollutant generation focused
mainly  on toxic pollutants such  as  cad-
mium,  cyanide, chromium, and chlorine.
Tables 2 and 3 show the changes in the
total waste and pollutant generation, re-
spectively.
  The increases in wastewater and sludge
were  due to  an increase in  plating bath
concentration from approximately 3 oz/gal
        of cadmium in the cadmium-plating baths
        to approximately 3.5  oz/gal zinc in the
        zinc-plating baths. The decrease in oil and
        grease was due to an approximately ten-
        fold  decrease in the concentration of oil
Table 2. Annual Generation of Treated Wastewater and Sludge from Cadmium- and Zinc-Plating
Processes (Aeroquip Data)
Year
1989
1991«»
Plating
Process
Cd
Zn
Treated
Wastewater,
gal
40,000,000
44,900,000
Sludge,
Ib
282,000
383,000
(a) Adjusted to the 1989 production rate of the electroplating process.
Table 3. Pollutant Generation from Cadmium- and Zinc-Plating Processes (Ib/yr based on production
rate of 3.29 million ft2)
             Pollutant
Cadmium Plating
                                                             Zinc Plating
Cd
Total CN
Total Cr
Zn
Oil & grease
12, 100
835
677
0
14,600
0
0
4,420
22,300
5,120

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used in the water-soluble oil dip tank. The
increase in chromium was due to an ap-
proximately fivefold increase in the chro-
mate bath  concentration. The chromium,
which also is a priority pollutant, was ef-
fectively  converted from  the  toxic
hexavalent form to a much less toxic triva-
lent form in the wastewater treatment plant;
therefore, it does not pose as great a
health  risk as does the cadmium. Thus,
the overall hazard level of the waste was
substantially reduced by eliminating cad-
mium and cyanide. The process substitu-
tion also eliminated the use  of chlorine
(95,900  Ib in 1989) for cyanide destruc-
tion  in  the wastewater treatment  plant.
Personnel  health risks were reduced sig-
nificantly by  eliminating  the handling  of
hazardous materials  such as cadmium,
cyanide, and chlorine. Consequently, the
process substitution  has reduced the
company's potential liability for accidental
worker exposure to and environmental re-
lease of these hazardous materials.

Economic Evaluation
   Economic evaluation of the process sub-
stitution  was based on a simple payback
period analysis  with the use  of the cost
data provided by Aeroquip. The evalua-
tion included  estimation of capital costs
for the process conversion and operating
costs of both processes. Table 4 shows
the capital cost (in 1992 dollars)  for con-
verting the plating lines at Aeroquip from
cadmium plating to zinc plating.
   Approximately 72% of the total cost was
for expenses related to cleaning up the
cadmium process equipment and for dis-
posal  of the  waste generated from the
cleanup operation; the remaining 28% was
for installing new equipment. Table  5
shows the annual operating cost  (in 1992
dollars) for the two plating processes. The
operating cost for the zinc-plating process
was slightly lower than that for the cad-
mium-plating process. For a new installa-
tion, therefore, the lower operating cost of
the zinc chloride plating process results in
an economic advantage over that of the
cadmium  cyanide plating process. The
payback period for the capital investment
required for converting  an existing cad-
mium-plating process to a zinc-plating pro-
cess was estimated at 115 yr. The process
conversion, therefore, cannot be justified
solely on economic grounds.  It should be
based on  worker safety and environmen-
tal pollution, as well as on greater accep-
tance of the zinc-plated components  in
domestic and foreign industrial and con-
sumer markets.
Table 4. Capital Cost to Convert (1992)
         Parameter
   Barrel
Plating Lines
   Hack
Plating Line
                                                            Subtotal
Expense (cleanup of old     $428,000        $999,000        $1,427,000
equipment and waste
disposal)

New equipment            $424,000        $122,000         $646,000
         Subtotal         $852,000        $1,121,000
           Total                                           $ 1,973,000
Table 5. Comparison of Operating Costs for Cadmium- and Zinc-Plating Processes (1992)
        Expenditure
               Cadmium
                Plating
                           Zinc
                          Plating
Electroplating chemicals
    Clear chromate                        $3,840
    Brightener                             3,180
    NaOH flakes                           3,330
    Yellow chromate                       16,900
    Sodium cyanide                        42,800
    Cadmium anode @ $0.99/lb              55,900
    Potassium chloride
    Boric acid
    Wetter
    Zinc anode @ $0.78/lb

Wastewater treatment chemicals            $215,000

Operating labor, 14 persons @ $25/hr        $728,000

Electricity, @ $0.08/kwh                     $8,920

Miscellaneous
    Blood tests          •                  $3,240
    Environmental monitoring                 2,320
    Record keeping                           463
    Washdown of plating dept.                6,370
    Treatment of washdown water             4,050

Sludge disposal cost, @ $178.50/ton          $ 25,200

Waste oil disposal, @ $600/drum              $15,600

Total                                 $1,135,000

Net cost reduction
                                            $49,800

                                              28,900


                                               6,1580
                                              18,200
                                               4,050
                                              46,000

                                           $ 190,000

                                           $ 728,000

                                              $ 7,880
                                             $34,200

                                              $3,600

                                          $1,118,000

                                             $ 17,200
 Conclusions
   The results from the corrosion tests per-
 formed in this study and  from historical
 data provided  by Aeroquip indicate that
 zinc-plated parts meet  customer require-
 ments of 96 hr of exposure to salt spray
 (ASTM Method B117-90)  before the ap-
 pearance of white corrosion products. Fur-
 ther, the zinc-plated  parts  meet the
 Aeroquip process requirements, of 360 hr
 of exposure to salt spray  before the ap-
 pearance of red rust. Although the corro-
                  sion  resistance properties  of  cadmium-
                  plated parts are superior to that of zinc-
                  plated parts, the corrosion  resistance of
                  zinc-plated parts can be considered satis-
                  factory to allow use of zinc as substitute
                  for cadmium in many plating applications.
                  The process substitution also satisfied the
                  requirements of some domestic and  for-
                  eign  customers for cadmium-free prod-
                  ucts.
                     The changes in the waste generation
                  from the process substitution were as fol-
                  lows:

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decrease of cadmium by 12,100 Ib/
yr.
decrease of cyanide by 835 Ib/yr,
decrease of oil  and grease  waste,
including waste oil, from 14,600 Ib/yr
to 5,120 Ib/yr,
increase of zinc by 22,300 Ib/yr,
increase  of chromium from  677 Ib/yr
to 4,420 Ib/yr,
increase  of treated wastewater from
40,000,000 gal/yr to 44,900,000 gal/
yr, and
increase of wastewater treatment
sludge from 282,000 Ib/yr to 383,000
Ib/yr.
  The use of chlorine for destruction of
cyanide in the wastewater treatment plant
was also eliminated.
  The capital cost for the process change
at  Aeroquip was  estimated to  be
$1,973,000. The annual operating cost re-
duction  that  resulted from the process
change was  estimated to be  $17,200.
Based on  these costs, the estimated
payback period is 115  yr. The process
change, therefore, cannot  be justified on
economic  grounds alone. Justification
would be based on the  improved worker
safety and reduced environmental pollu-
tion  plus  the market's requirements for
zinc-plated rather than cadmium-plated
parts in many applications.  In comparing
the two processes for a new installation,
the zinc chloride plating process offers
obvious advantages over the cadmium
cyanide plating process.
  The full report was submitted in partial
fulfillment of Contract Number 68-CO-0003,
Work Assignment 3-36, under the Spon-
sorship of the U.S. Environmental Protec-
tion Agency.
                                                               •&IU.S. GOVERNMENT PRINTING OFFICE: MM - SSO-067/80247

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B.C. Kim, P.R. Webb, J.A. Gurklis, and R.K. Smith are with Battelle, Columbus,
  OH 43201-2693.
Teresa Harten is the EPA Project Officer (see below).
The complete report, entitled "Substituting Cadmium Cyanide Electroplating
    with Zinc Chloride Electroplating," (Order No. PB94-165321; Cost: $19.50
    subject to change) will be available only from
        National Technical Information Service
        5285 Port Royal Road
        Springfield, VA 22161
        Telephone: 703-487-4650
The EPA Project Officer can be contacted at
        Risk Reduction Engineering Laboratory
        U.S. Environmental Protection Agency
        Cincinnati, OH 45268
   United States
   Environmental Protection Agency
   Center for Environmental Research Information
   Cincinnati, OH 45268

   Official Business
   Penalty for Private Use
   $300
      BULK RATE
POSTAGE & FEES PAID
         EPA
   PERMIT No. G-35
   EPA/600/SR-94/074

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