United States Environmental Protection Agency Risk Reduction Engineering Laboratory Cincinnati, OH 45268 Research and Development EPA/600/SR-94/074 May 1994 EPA Project Summary Substituting Cadmium Cyanide Electroplating with Zinc Chloride Electroplating B.C. Kim, P.R. Webb, J.A. Gurklis, and R.K. Smith The environmental and economic im- plications of substituting zinc chloride electroplating for cadmium cyanide electroplating were evaluated. The pro- cess substitution successfully achieved product quality to satisfy the customer requirements for corrosion resistance. Corrosion resistance was determined by salt-spray tests in accordance with the ASTM Method B117-90. Not only did the process substitution eliminate cadmium and cyanide from the wastes and chlorine from the wastewater treat- ment process, thereby greatly reduc- ing hazards to plant personnel and pollution of the environment, the pro- cess substitution also reduced oil and grease waste. On the negative side, however, the process change increased the generation of wastewater, waste- water treatment sludge, and chromium. For a new installation, the zinc-plating process offers an economic advantage of slightly lower operation cost over the cadmium-plating process. This Project Summary was developed by EPA's Risk Reduction Engineering Laboratory, Cincinnati, OH, to announce key findings of the research project that is fully documented in a separate report of the same title (see Project Report ordering information at back). Introduction This study, performed under the U.S. Environmental Protection Agency's (EPA's) Waste Reduction Innovative Technology Evaluation (WRITE) Program, was a co- operative effort between EPA's Risk Re- duction Engineering Laboratory (RREL) and Aeroquip Corporation. The objective of the WRITE program is to evaluate, in a typical workplace environment, examples of prototype technologies that have po- tential for reducing wastes. Substitution of zinc chloride electroplating for cadmium cyanide electroplating was evaluated at Aeroquip's Industrial Connectors Division* in Van Wert, OH. The goal of this project was to evaluate (1) the effects of the pro- cess substitution on product quality, (2) the waste reduction/pollutant reduction ef- fects of the process substitution, and (3) the economics of the process substitution. The Processes The cadmium cyanide and the zinc chlo- ride plating processes for the rack plating line at Aeroquip are compared in Table 1. Hydrochloric acid is used to condition parts (shown as step 12 in Table 1) before plating in the zinc chloride process whereas sodium cyanide is used in the cadmium cyanide process. The cadmium cyanide plating line had separate tanks to apply either clear chromate or yellow chro- mate coatings (steps 18 and 20 in Table 1). Previously, Aeroquip used clear chro- mate coating on most (90% to 95%) of the cadmium-plated parts. Currently, Aeroquip uses yellow chromate coating on all zinc-plated parts because (1) Aeroquip has adopted a worldwide stan- dardization of yellow as the color for their fittings and (2) yellow chromate coating vastly improves the corrosion protection * Mention of trade names or commercial products does not constitute endorsement or recommendation for use. Printed on Recycled Paper ------- Tab/a 1. Comparison of Zinc Chloride and Cadmium Cyanide Back Plating Processes Operation Process Step 1 2 3 4 5 6 7 8 9 10 11 12 13 14 15 16 17 18 19 20 21 22 Tank No. 1 2 3 4 5 6 7 8 9 10 11 12 13 14 15 16 17 18 19 20 21 '22 Zinc Chloride Plating Line Soak clean Rinse Electroclean Rinse Rinse Hydrochloric acid pickle Rinse Rinse Electroclean Rinse Rinse Hydrochloric acidpre-dip Zinc plating Rinse Rinse Nitric acid dip Yellow chromate dip Rinse Chromate seal Rinse Drip tank dip Water-soluble oil dip Cadmium Cyanide Plating Line Soak clean Rinse Electroclean Rinse Rinse Hydrochloric acid pickle Rinse Rinse Electroclean Rinse Rinse Sodium cyanide pre-dip Cadmium plating Rinse Rinse Rinse Nitric acid dip Clear chromate dip Rinse Yellow chromate dip Rinse Water-soluble oil dip of the zinc-plated fittings. The yellow chro- mate solution used by Aeroquip contained approximately a five times greater chro- mium concentration than did the clear chro- mate solution. In the water-soluble oil application step (step 22 in Table 1), the concentration of the oil was reduced by a factor of approximately ten in the zinc chloride plating process from the level used In the cadmium cyanide plating process. The change was necessary to obtain im- proved adhesion of chromate coating dur- ing the subsequent heat-curing step. Rinse water and various cleaning and plating solutions are discharged continu- ously or periodically dumped from the tanks and treated in an on-site wastewa- ter treatment plant. All wastes from the plating operations eventually are in three waste streams — treated wastewater, de- watered sludge, and waste oil — that are discharged or disposed from the waste- water treatment plant. The treated waste- water is discharged to a sanitary sewer. The dewatered sludge is collected in a 20-yd3 hopper and sent to an off-site haz- ardous landfill once a month. The waste oil Is collected in drums and sent to an off-site hazardous waste incinerator every 3 mo. Product Quality Evaluation Product quality was measured by the corrosion resistance of plated parts deter- mined by salt-spray (fog) tests carried out In accordance with the ASTM Method B117-90 (Standard Test Method of Salt Spray [Fog] Testing). As part of their qual- ity acceptance criteria for zinc-plated parts, Aeroquip's engineering process specifica- tion has adopted the ASTM Method B633- 85 (Standard Specification for Electro- deposited Coatings of Zinc on Iron and Steel) requirement of 96 hr of freedom from white corrosion products in salt-spray testing. Most Aeroquip customers require 96 hr before the first appearance of white corrosion on zinc-plated parts. The pro- cess specification for some of Aeroquip's products has an additional internal accep- tance criterion (not required by custom- ers) of 360 hr of exposure to salt spray before the first appearance of red rust. In the first series of tests, four repre- sentative types of parts plated with zinc in the rack plating line were tested in parallel by Aeroquip and an independent testing laboratory (Detroit Testing Laboratory, Inc. [DTL], Warren, Ml). These parts, shown in Figure 1, included swivel nut (Group B) and three types of adapter (Groups A, C, and D). In the DTL tests, all of the Group A, B, and D specimens were free of white corrosion products at 120 hr, so that the 96-hr requirement of no white corrosion for zinc-plated parts was met. Very slight white corrosion was noted on some Group C specimens at 120 hr. In the DTL tests, all specimens in Groups A, B, and D were free of red rust at the end of the 360-hr observation period; two of the six speci- mens in Group C showed red rust at the 336-hr and 360-hr observation periods. In the Aeroquip tests, there was no sign of white corrosion products on any of the specimens in any of the groups at the 96- hr observation period. Further, the ex- tended-exposure tests showed that only one of six specimens in Group D exhib- ited red rust at 264 hr. Thus, of a total 24 specimens tested by Aeroquip, only one specimen definitely would not have met Aeroquip's internal requirement of free- dom from red rust at 360 hr. One speci- men in Group B exhibited!red rust at 408 hr; at 336 hr, no specimens in this group showed red rust. In general, very good agreement and full compliance with the requirement for absence of white corro- sion products for 96 hr was noted for the groups of specimens tested at both labo- ratories. Further, there was generally good agreement in results with respect to the appearance of red rust. At both laborato- ries, only 3 of 48 specimens did not meet the Aeroquip's internal requirement of free- dom from red rust for 360 hr of exposure to salt-spray. Aeroquip also tested four groups of parts platedjwith zinc in the barrel plating lines. The parts included nipple (Group A), crimp socket (Group B), and two other types of socket (Groups C and D). All specimens in all four groups met the requirement of freedom from white corrosion products at 96 hr. White corrosion started to appear on most of the specimens at the 168-hr observation point. All parts also met the requirement of no red rust at 360 hr. One specimen in Group A exhibited red rust at 432 hr. At 504 hr, red rust was present on Group A and Group C parts, but Group B and Group D specimens showed no red rust. From October 15 to November 5, 1991, Aeroquip carried out corrosion tests to compare the salt-spray corro- sion resistance of zinc-plated parts with cadmium-plated parts. Seven groups of representative parts plated with zinc and " seven groups of identical parts plated with cadmium were tested. The parts included two types of barrel-plated reus- able sockets (Groups A and B), two types of barrel-plated reusable nipples (Groups C and D), two types of rack plated nuts (Groups E and F), and a rack-plated crimp fitting (Group G). The results of the salt- spray tests on the zinc-plated parts were as follows: (1) all specimens in the seven groups of parts passed the requirement of 96 hr before the first appearance of white corrosion products; (2) no red rust ap- peared on any of the specimens in the seven groups at the 360-hr observation time; (3) all specimens in Groups A, B, D, and G were still free of red rust after 504 hr of salt-spray exposure; red rust was ------- Group A: Part No. 2021-2-35; Pipe to 37 ° mate Hare adapter Group B: Part No. 210204-12s; swivel nut (crimp type) Group C: Part No. 206204-8-6s; SAE male to 37' male flare adapter Group D: Part No. 2089-6-6s; 90 ° male to female pipe adapter Figure 1. Zinc-plated parts salt-spray tested by Detroit Testing Laboratory andAeroquip (rack plated). beginning to develop on specimens in Groups C, E, and F at 504 hr. The results of the salt-spray tests on cadmium-plated parts were as follows: (1) all specimens in the seven groups passed the requirement of 96 hr before the first appearance of white corrosion products, and the appear- ance of white corrosion products in any of the seven groups was delayed to 336 hr and beyond and (2) no red rust was ob- served on any of the cadmium-plated specimens after 504 hr of exposure, at which point the tests were ended. These results demonstrated that the cadmium- plated parts exhibit superior corrosion re- sistance to zinc-plated parts with regard to the appearance of white corrosion prod- ucts and red rust in salt-spray tests. Waste Reduction Potential Waste reduction potential of the pro- cess substitution was determined on the basis of waste volume reduction and pol- lutant reduction. Waste volume reduction was estimated for the treated wastewater and the dewatered sludge, which, respec- tively, affect conservation of water and landfill space. Pollutant generation focused mainly on toxic pollutants such as cad- mium, cyanide, chromium, and chlorine. Tables 2 and 3 show the changes in the total waste and pollutant generation, re- spectively. The increases in wastewater and sludge were due to an increase in plating bath concentration from approximately 3 oz/gal of cadmium in the cadmium-plating baths to approximately 3.5 oz/gal zinc in the zinc-plating baths. The decrease in oil and grease was due to an approximately ten- fold decrease in the concentration of oil Table 2. Annual Generation of Treated Wastewater and Sludge from Cadmium- and Zinc-Plating Processes (Aeroquip Data) Year 1989 1991«» Plating Process Cd Zn Treated Wastewater, gal 40,000,000 44,900,000 Sludge, Ib 282,000 383,000 (a) Adjusted to the 1989 production rate of the electroplating process. Table 3. Pollutant Generation from Cadmium- and Zinc-Plating Processes (Ib/yr based on production rate of 3.29 million ft2) Pollutant Cadmium Plating Zinc Plating Cd Total CN Total Cr Zn Oil & grease 12, 100 835 677 0 14,600 0 0 4,420 22,300 5,120 ------- used in the water-soluble oil dip tank. The increase in chromium was due to an ap- proximately fivefold increase in the chro- mate bath concentration. The chromium, which also is a priority pollutant, was ef- fectively converted from the toxic hexavalent form to a much less toxic triva- lent form in the wastewater treatment plant; therefore, it does not pose as great a health risk as does the cadmium. Thus, the overall hazard level of the waste was substantially reduced by eliminating cad- mium and cyanide. The process substitu- tion also eliminated the use of chlorine (95,900 Ib in 1989) for cyanide destruc- tion in the wastewater treatment plant. Personnel health risks were reduced sig- nificantly by eliminating the handling of hazardous materials such as cadmium, cyanide, and chlorine. Consequently, the process substitution has reduced the company's potential liability for accidental worker exposure to and environmental re- lease of these hazardous materials. Economic Evaluation Economic evaluation of the process sub- stitution was based on a simple payback period analysis with the use of the cost data provided by Aeroquip. The evalua- tion included estimation of capital costs for the process conversion and operating costs of both processes. Table 4 shows the capital cost (in 1992 dollars) for con- verting the plating lines at Aeroquip from cadmium plating to zinc plating. Approximately 72% of the total cost was for expenses related to cleaning up the cadmium process equipment and for dis- posal of the waste generated from the cleanup operation; the remaining 28% was for installing new equipment. Table 5 shows the annual operating cost (in 1992 dollars) for the two plating processes. The operating cost for the zinc-plating process was slightly lower than that for the cad- mium-plating process. For a new installa- tion, therefore, the lower operating cost of the zinc chloride plating process results in an economic advantage over that of the cadmium cyanide plating process. The payback period for the capital investment required for converting an existing cad- mium-plating process to a zinc-plating pro- cess was estimated at 115 yr. The process conversion, therefore, cannot be justified solely on economic grounds. It should be based on worker safety and environmen- tal pollution, as well as on greater accep- tance of the zinc-plated components in domestic and foreign industrial and con- sumer markets. Table 4. Capital Cost to Convert (1992) Parameter Barrel Plating Lines Hack Plating Line Subtotal Expense (cleanup of old $428,000 $999,000 $1,427,000 equipment and waste disposal) New equipment $424,000 $122,000 $646,000 Subtotal $852,000 $1,121,000 Total $ 1,973,000 Table 5. Comparison of Operating Costs for Cadmium- and Zinc-Plating Processes (1992) Expenditure Cadmium Plating Zinc Plating Electroplating chemicals Clear chromate $3,840 Brightener 3,180 NaOH flakes 3,330 Yellow chromate 16,900 Sodium cyanide 42,800 Cadmium anode @ $0.99/lb 55,900 Potassium chloride Boric acid Wetter Zinc anode @ $0.78/lb Wastewater treatment chemicals $215,000 Operating labor, 14 persons @ $25/hr $728,000 Electricity, @ $0.08/kwh $8,920 Miscellaneous Blood tests • $3,240 Environmental monitoring 2,320 Record keeping 463 Washdown of plating dept. 6,370 Treatment of washdown water 4,050 Sludge disposal cost, @ $178.50/ton $ 25,200 Waste oil disposal, @ $600/drum $15,600 Total $1,135,000 Net cost reduction $49,800 28,900 6,1580 18,200 4,050 46,000 $ 190,000 $ 728,000 $ 7,880 $34,200 $3,600 $1,118,000 $ 17,200 Conclusions The results from the corrosion tests per- formed in this study and from historical data provided by Aeroquip indicate that zinc-plated parts meet customer require- ments of 96 hr of exposure to salt spray (ASTM Method B117-90) before the ap- pearance of white corrosion products. Fur- ther, the zinc-plated parts meet the Aeroquip process requirements, of 360 hr of exposure to salt spray before the ap- pearance of red rust. Although the corro- sion resistance properties of cadmium- plated parts are superior to that of zinc- plated parts, the corrosion resistance of zinc-plated parts can be considered satis- factory to allow use of zinc as substitute for cadmium in many plating applications. The process substitution also satisfied the requirements of some domestic and for- eign customers for cadmium-free prod- ucts. The changes in the waste generation from the process substitution were as fol- lows: ------- decrease of cadmium by 12,100 Ib/ yr. decrease of cyanide by 835 Ib/yr, decrease of oil and grease waste, including waste oil, from 14,600 Ib/yr to 5,120 Ib/yr, increase of zinc by 22,300 Ib/yr, increase of chromium from 677 Ib/yr to 4,420 Ib/yr, increase of treated wastewater from 40,000,000 gal/yr to 44,900,000 gal/ yr, and increase of wastewater treatment sludge from 282,000 Ib/yr to 383,000 Ib/yr. The use of chlorine for destruction of cyanide in the wastewater treatment plant was also eliminated. The capital cost for the process change at Aeroquip was estimated to be $1,973,000. The annual operating cost re- duction that resulted from the process change was estimated to be $17,200. Based on these costs, the estimated payback period is 115 yr. The process change, therefore, cannot be justified on economic grounds alone. Justification would be based on the improved worker safety and reduced environmental pollu- tion plus the market's requirements for zinc-plated rather than cadmium-plated parts in many applications. In comparing the two processes for a new installation, the zinc chloride plating process offers obvious advantages over the cadmium cyanide plating process. The full report was submitted in partial fulfillment of Contract Number 68-CO-0003, Work Assignment 3-36, under the Spon- sorship of the U.S. Environmental Protec- tion Agency. •&IU.S. GOVERNMENT PRINTING OFFICE: MM - SSO-067/80247 ------- ------- ------- B.C. Kim, P.R. Webb, J.A. Gurklis, and R.K. Smith are with Battelle, Columbus, OH 43201-2693. Teresa Harten is the EPA Project Officer (see below). The complete report, entitled "Substituting Cadmium Cyanide Electroplating with Zinc Chloride Electroplating," (Order No. PB94-165321; Cost: $19.50 subject to change) will be available only from National Technical Information Service 5285 Port Royal Road Springfield, VA 22161 Telephone: 703-487-4650 The EPA Project Officer can be contacted at Risk Reduction Engineering Laboratory U.S. Environmental Protection Agency Cincinnati, OH 45268 United States Environmental Protection Agency Center for Environmental Research Information Cincinnati, OH 45268 Official Business Penalty for Private Use $300 BULK RATE POSTAGE & FEES PAID EPA PERMIT No. G-35 EPA/600/SR-94/074 ------- |