United States
           Environmental Protection
           Agency
Center for Environmental
Research Information
Cincinnati, OH 45268
EPA/625/8-90/017
March 1990
           Technology Transfer
v>EPA     Summary Report

           Optimizing Water
           Treatment Plant
           Performance with the
           Composite Correction
           Program

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                                    EPA/625/8-90/017
                                      March 1990
         Summary Report


Optimizing Water Treatment Plant
       Performance with the
  Composite Correction Program
        U.S. Environmental Protection Agency
        Office of Research and Development

     Center for Environmental Research Information
             Cincinnati, OH 45268

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                                        Notice
This document has  been reviewed  in accordance  with the  U.S.  Environmental  Protection
Agency's peer and administrative review policies and  approved for publication. Mention of trade
names or commercial products does not constitute endorsement or recommendation for use.

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                                  Contents
Section
                                                                        Page
 1   INTRODUCTION  	           1

    Purpose 	            1
    Background	  1
    Content	  1

2   THE COMPOSITE CORRECTION PROGRAM	  3

    The Comprehensive Performance Evaluation  	     3
    The Composite Correction Program	       6

3   RESULTS OF CASE STUDIES  	  g

    CPE Findings 	                              g
    CCP Findings 	'.'.'.'.'.'.'.'.'.'.'.'.'.'.'.'.	12
    Overall Factors Limiting Performance	  12


4   CASE STUDIES  	  15

    Plant 1 	                                              1C;
    Plant 2	               	  21
    Plant 3	              	       pn
    Plant 4	            	  34
    piant 5	;;;;;	  40
    Plant 6	                      	  ?a
    Plant 7	             	  53
   Plant 8 	                  	  cq
   Plant 9	              	  57
   Plant 10 	               	  70
   Plant 11  	      	  a?
   Plant 12 	           	  o7
        13	!:.'.'::::::::::::::::::::::  95

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                               Acknowledgments
Although many  individuals  contributed to the preparation  and review  of this  document,  the
assistance of the individuals listed  below is especially acknowledged. Those who assisted by
participating in the actual field  studies described in the document are noted below as "Onsite
Reid Participants."

Major Authors:
    Robert C. Renner and Bob  A. Hegg, Process Applications, Inc., Ft. Collins, Colorado
    Jon H. Bender, EPA Technical Support Division (TSD), Cincinnati, Ohio

Technical Writing and Editing:
    Heidi Schultz and Susan Richmond, Eastern Research Group, Inc., Arlington, Massachusetts

Project Managers:
    Jon H. Bender, EPA TSD, Cincinnati,  Ohio
    James E. Smith, EPA Center for Environmental Research Information (CERI),
        Cincinnati, Ohio

Reviewers:
    Eric Bissonette, EPA TSD,  Cincinnati, Ohio
    Robert Blanco, EPA Office  of Drinking Water (ODW), Washington, D.C.
    Peter Cook, EPA ODW, Washington, D.C.
    Dan Fraser, Montana Department of Health and Environmental Sciences (DHES),
        Helena, Montana
    Denis J. Lussier, EPA CERI, Cincinnati,  Ohio
    James Westrick, EPA TSD, Cincinnati, Ohio

Onsite Reid Participants:

EPA
    Jon H. Bender, EPA TSD,  Cincinnati, Ohio
    Eric Bissonette, EPA TSD,  Cincinnati, Ohio
    Dean Chaussee, EPA Region VIII, Helena, Montana
    Ben W. Lykins,  EPA, Office of Research and Development,  Cincinnati, Ohio
    James E. Smith, EPA CERI, Cincinnati,  Ohio
    James Westrick, EPA TSD, Cincinnati, Ohio

State of Montana
    Dave Aune, Montana DHES, Helena,  Montana
    Jerry Burns, Montana DHES, Billings, Montana
    Dan Fraser, Montana, DHES, Helena, Montana
    Donna Howell, Montana DHES, Helena, Montana
    Denise Ingman, Montana DHES, Helena, Montana
    James Melsted,  Montana DHES, Helena, Montana
    Kate Miller, Montana DHES, Billings, Montana
    Rick Rosa, Montana DHES, Helena, Montana
    Mark Smith, Montana DHES, Helena, Montana
    Roy Wells, Montana DHES, Helena, Montana
                                          IV

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State of Ohio
   Gary Cutler, Ohio EPA, Columbus, Ohio
   Steve Severyn, Ohio EPA, Columbus, Ohio

State of Kentucky
   Fred Cooper, Kentucky Department of Environmental Protection (DEP), Morehead, Kentucky
   George Schureck, Kentucky DEP, Frankfort, Kentucky
   Tom Stern, Kentucky DEP, Frankfort, Kentucky
   Damon White, Kentucky DEP, Hazard, Kentucky

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                                             SECTION 1

                                         INTRODUCTION
 Purpose

 This document summarizes the results of an ongoing
 project to evaluate  the  utility of the  Composite
 Correction Program (CCP) approach to improving the
 performance of drinking water treatment facilities. The
 CCP approach, which has already  proven successful
 when  applied  to  wastewater  treatment plants,  is
 described and the results  of evaluating  it at  13
 drinking water plants to date are summarized.

 The 13 "case studies" focus on the potential for the
 CCP approach to  improve the performance  of small
 drinking  water systems in  meeting the  turbidity
 removal requirements of the Surface Water Treatment
 Rule (SWTR).

 The CCP approach is still  under development. The
 end product of this project will be  a  publication that
 describes the  refined CCP approach and  allows it to
 be applied by others.

 Background

 Many  communities  are  now  considering either
 construction of new facilities or major modifications to
 existing ones to meet drinking water  regulations. An
 approach that  allows communities to meet regulatory
 requirements  by  implementing changes  in their
 operation,  maintenance,  and  administration
 procedures instead of major capital improvements has
 obvious advantages. By maximizing the  operational
 efficiency  of their  facilities, local administrators can
 both improve the ability of the facility to  meet Safe
 Drinking  Water  Act  (SDWA)  requirements  and
 minimize  the  financial  impact to the  community
 associated with major upgrades to the plant.

 Recognizing  that  the CCP  approach   had  been
 successfully  developed  and  applied  to small
wastewater treatment plants to accomplish the same
objectives, the State of Montana decided  to evaluate
the  potential of modifying it for use at small  drinking
water  plants.  Based on the  initial  success  of  this
evaluation, U.S. EPA decided to further develop and
demonstrate the approach to ensure its applicability  to
other parts of the country.
 Since 88 percent of the 60,000 community drinking
 water systems in the United States are small systems
 serving fewer than 3,300 individuals, the opportunity
 for  widespread  impacts  are large. These  small
 systems account for approximately 92 percent of the
 SDWA  compliance problems  reported each year. In
 1987, more than 80 percent of the community drinking
 water systems  experiencing  significant compliance
 difficulties were small systems.

 Small systems  frequently can  neither readily identify
 and address  the factors that cause their compliance
 problems nor easily finance  the  upgrading of  their
 facilities. The staff may be inadequate  in  numbers,
 experience  and  training to  effectively solve  the
 problems. Successful application  of the  CCP
 approach can identify  cost-effective measures  that
 can be  taken to improve  plant performance  and
 comply with drinking water requirements.

 The CCP approach is another tool that federal, state,
 or  local  regulators,  technical  personnel,  and
 consultants familiar with the  procedure  can use to
 identify  and  correct  factors  that limit a plant's
 performance.  Results to date  suggest that it is  both
 highly successful and cost effective.

 Content

 Section 2 of this document details the CCP approach,
 including facility review, performance analysis,  and
 implementation  of corrective  measures.  Section 3
 summarizes  the  results of  the  case   studies,
 highlighting  specific  instances  where the  CCP
 approach revealed problems that were not previously
obvious to drinking water treatment plant operators.
Also  highlighted are  instances  where the  CCP
approach saved  the facilities  money that otherwise
would have been spent in plant modification. Section
4 includes expanded  information on the   13  case
studies that have been  conducted to date should  the
reader desire additional information.

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                                             SECTION 2

                  THE COMPOSITE CORRECTION PROGRAM APPROACH
 The CCP  approach consists of a  Comprehensive
 Performance  Evaluation  (CPE)  and  a Composite
 Correction  Program (CCP). The CPE is a systematic
 step-by-step evaluation of an existing treatment plant
 resulting in a comprehensive assessment of the unit
 treatment process capabilities and the  impact  of the
 operation,  maintenance and  administrative practices
 on performance of the plant.

 It  is  conducted  by  a  team of individuals with
 knowledge  of drinking water treatment  and  results in
 the identification of a unique  combination of factors
 limiting  plant performance. This  team   reviews  and
 analyzes the plant's physical capacity  as well  as its
 operational capability and associated maintenance and
 administration.  Based  on  this  analysis, the team
 projects the capabilities of the major unit processes
 within the  plant, and  identifies and prioritizes  those
 factors affecting plant performance.

 If the CPE indicates that optimization of  existing major
 unit processes can result  in  desired finished  water
 quality,  the CCP  phase is implemented. The  CCP
 systematically addresses those factors  identified  and
 prioritized in the CPE phase.

 Figure 2-1  graphically  illustrates  the CPE/CCP
 approach. The CPE team usually is composed of two
 individuals experienced  in the  design and operation of
 drinking  water treatment  facilities and in trouble
 shooting  their  operation.  Teams  composed of  up to
 seven individuals were  employed  for  each of the 13
 case studies described in this document, although it is
 anticipated that teams this large will not  be required to
apply  the finalized  CPE/CCP  approach. These  larger
teams were used to help evaluate and  further  refine
the procedure as well  as  familiarize regulatory
personnel with it.

The Comprehensive Performance
 Evaluation

The CPE begins with a plant tour and collection of
information  from  plant records. Data are obtained by
interviewing  plant staff and key  administrative
personnel  (for example,  the  mayor and other city
administrators),  reviewing the  plant's physical
capacity,  examining  the  plant's  operation  and
 maintenance records,  and  reviewing  budgets.
 Standardized forms are used to collect the data on
.raw and treated water quality, design and operating
 conditions for individual  plant processes, plant
 operator coverage, user fees for water  treatment,
 maintenance  scheduling,  and  operating  budgets.
 While the data collection efforts focus on the current
 status of the plant, the review also includes past
 records  to account for  factors such as  seasonal
 variations in raw water  quality and peak demand,  and
 to establish an accurate record of plant performance.

 In addition to gathering existing  data, the CPE may
 involve  collecting  new data by  conducting  special
 studies. For example, the CPE team usually develops
 a  turbidity vs. time profile on a  plant's filters  before
 and after backwashing to determine whether the filters
 were  performing  adequately (see  Figure 2-2).  At
 nearly all plants,  such  a profile revealed  that  a
 significant breakthrough of turbidity occurred after the
 backwash. When the CPE team sampled the clearwell
 at one end,  they  discovered turbidity values  of  6.3
 NTU, which clearly exceeded the regulatory criteria.
 Other special studies conducted  as part of the CPE
 often  reveal similar performance problems  that may
 not be obvious to the plant staff.

 Design Components
 The CPE team  determines a  plant's capacity by
reviewing  plant drawings and specifications,  making
field  measurements,  and  reviewing  information
provided  by  the plant  staff.  In  addition,  the team
applies its experience based on evaluations performed
at other plants. The CPE  evaluators  then determine
the projected capacity at  which  plant  major unit
processes (flocculation, sedimentation, filtration, and
disinfection)  can provide acceptable  treated  water
quality. Projected  values are compared  with peak
instantaneous  operating capacity and current plant
production. The comparison results are  summarized
using  a performance potential graph (see Figure 2-3),
which illustrates the strengths and weaknesses of  the
plant's unit processes.

Operation and Maintenance
Operational  factors are assessed  by  evaluating
procedures that the plant uses  for process  control
adjustments  and by determining if steps the plant

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I
           Figure 2-1    CPE/CCP schematic of activities.
                                                          Administrators
                                                        Recognize Need To
                                                     Improve Plant Performance
                                                         CPE Evaluation
                                                              of
                                                       Major Unit Processes
                     Major Unit Processes
                           Are
                         Adequate
  Major Unit Processes
        Are
      Marginal
                     Implement CCP to
                      Achieve Desired
                        Performance
                    From Existing Facilities
 Major Unit Processes
        Are
     Inadequate
   Implement CCP to
Optimize Existing Facilities
    Before Initiating
  Facility Modifications
Do Not Implement CCP
  Evaluate Options For
  Facility Modifications
                                                    Desired Performance Achieved
                                                                                                   Abandon Existing
                                                                                                     Facilities and
                                                                                                       Design
                                                                                                      New Ones
           takes to modify operations  are based  on  proper
           application  of water treatment concepts and methods.
           The CPE team discusses process control measures in
           detail with plant operators. This enables  them to
           accurately  assess the plant's operation  and to avoid
           any  misunderstandings  related to  terminology.
           Maintenance  capabilities are  evaluated  by reviewing
           maintenance  schedules and records, observing spare
           parts inventories, observing the condition  of plant
           equipment, and discussing maintenance  activities  with
           plant personnel.

           Administration
           The  CPE  evaluators  interview  plant operators  and
           administrative personnel (for example, city managers,
           town clerks,  water board  officials,  etc.) to consider
           administrative  factors such  as staffing  (including
           training, motivation,  and  morale), budgets,  and  rate
           structures.

           Evaluating the  Factors that Limit Performance
           After critically studying the plant  design, performance,
           maintenance, administration and  operation,  the CPE
           team assesses  the  performance  of the plant  and
           conducts an  in-depth  analysis to identify the specific
            factors  that limit  this  performance.  They  use  a
            checklist  containing  more  than  65  performance-
            limiting factors (see Table 2-1) and define each factor
            according  to  its  specific  cause  of  poor  plant
            performance. Once the  factors have been identified,
            they are prioritized according to the magnitude of their
            adverse  effects on plant  performance. This is  the
            major  output from  a  CPE:  a  prioritized  list  of
            performance limiting factors.

            Reporting
            The CPE  team conducts an  exit  meeting  with
            administrative  and  operations  personnel  to
            communicate the  results of the  CPE  directly to  all
            concerned.  This is  followed  up with a brief written
            report. The  purpose of the report is to summarize the
            results of the  CPE  and list  the  prioritized  factors
            limiting plant performance. A typical CPE report is 8 to
            12 pages in length and addresses the following topics:
               Facility description
               Major unit process evaluation
               Performance assessment
               Performance-limiting factors
               Projected impact of a CCP

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                                Figure 2-2.   Filter effluent turbidity profile.

                                  Turbidity, NTU

                                     40  r-
                                      10  -
                                                                       Present Requirements
                                                               15      20

                                                              Minutes
Figure 2-3.   Sample performance potential graph.


     Unit Process
     Flocculation1

       HOT, min


     Sedimentation2
       SOR, gpd/sq ft


     Filtration3
       HLR, gpm/sq ft


     Disinfection4
       Contact time,  min
                                                  0.2
    Flow, mgd
0.4           0.6
                                                                                           0.8
                                                                                                         1.0

113 57 38 28

150 302 452 603

0.4 0.7 1.1 1.5

180 90 60


23



1.8 2.2 2.5 2.! I



                                                      Peak Instantaneous Operating Flow
                                                        Rate, One Pump = 300 gpm


   1 Rated at 20 min - assumes variable speed drive would be added.
   2 Rated at 750 gpd/sq ft - 12.5-ft depth discourages higher rating.
   3 Rated at 3 gpm/sq ft - control system considered limiting.
   4 Rated at CT = 127 with 2.4 mg/L CI2 dose, which requires a 53-min HOT; CT based on 4 log required reduction - 2.5 log in plant; 1.5
     log disinfection, pH  = 8, temperature =  5ฐC. Assumes 10% of usable clearwell volume for contact time..

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 Table 2-1.   Performance-Limiting Factors
 Table 2-1.   Performance-Limiting Factors (continued)
 ADMINISTRATION
 Plant Administrators
   - Policies
   - Familiarity with plant needs
   - Supervision
   - Planning
 Plant Staff
   - Manpower
    • number
    - plant coverage
    - work load distribution
    - personnel turnover
   - Morale
    - motivation
    -pay
    - work environment
   - Staff qualifications
    - aptitude
    - level of education
    - certification
   - Productivity
 Financial
   - Insufficient funding
   - Unnecessary expenditures
   - Bond indebtedness
 Water Demand

 MAINTENANCE
 Preventive
   - Lack of program
   • Spare parts inventory
 Corrective
   - Procedures
   - Critical parts procurement
 General
   - Housekeeping
   - References available
   - Staff expertise
   • Technteal guidance
   - Equipment age
A CPE report does not recommend specific actions to
be  taken  to correct  individual  performance-limiting
factors,  since this  could lead to  a piecemeal rather
than  an integrated  approach to  corrective  actions.
Corrective actions  should be  undertaken  in the  next
phase - the  CCP - with the help of the  CPE team or
similarly experienced individuals.

The Composite Correction Program

The  objective of  this phase  is to  improve   the
performance  of a drinking water treatment plant by
implementing the  findings  of  the  CPE  when it
indicates that the  plant  is  likely to  meet treatment
requirements with the existing major unit processes.
The CCP  focuses on  systematically addressing  the
factors that  limit the  plant  in achieving the  desired
finished water quality.

Implementing the Composite Correction Program
To  successfully  implement the  CCP  and  achieve
improved performance, facilities  must utilize the CPE
results and  implement a long-term  process  control
  DESIGN
  Raw Water
   - THM precursors
   - Turbidity
   - Seasonal variation
   - Watershed/Reservoir management
  Unit Design Adequacy
   - Pretreatment
    -  intake structure
    -  pre-sedimentation basin
    -  pre-chlorination
   - Low service pumping
   - Flash mix
   - Flocculation
   - Sedimentation
   - Filtration
   - Disinfection
   - Sludge treatment
   - Ultimate sludge disposal
   - Fluoridation
  Miscellaneous
   - Process flexibility
   - Process controllability
   - Process automation
   - Lack of standby units for key equipment
   - Flow proportioning units
   - Alarm systems
   - Alternate power source
   - Laboratory space and equipment
   - Sample taps
   - Plant inoperability due to weather
   - Return process streams

 OPERATION
 Testing
   - Performance monitoring
   - Process control testing
 Process Control Adjustments
   - Water treatment understanding
   - Application of concepts and testing to process control
   - Technical guidance (operations)
   - Training
   - Insufficient time on job
 O&M Manual/Procedure
   - Adequacy
   -Use
 Distribution System

 MISCELLANEOUS
program. A factor  in  any  one  of the  performance-
limiting  areas  (design, maintenance,  administration,
and operation) can  contribute to poor  performance.  It
is  unlikely, however,  that a  single factor  limits
performance; rather it is usually a  unique combination
of  factors  that causes  poor  water quality.  Plant
operators  and  administrators  must understand  the
relationship among  these areas  and  water treatment
plant product water quality. It is the operation  of the
plant  that  enables a  physically  capable  plant to
produce adequately treated water.

Maintaining Long-Term Involvement
One of  the keys,  as  already  noted,  to  successfully
implementing  a CCP  program  is  long-term  effort

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(typically involving several months to a year).  Long-
term involvement is critical for several reasons:

• Repeat training is more effective than one-time only
  training.  Training should  be conducted  under  a
  variety of operating and  administrative conditions
  (for example,  when seasonal water  quality  or
  demand  changes)  in order  for staff  to   develop
  confidence in new techniques or procedures.

• Time is  required to make the  necessary  physical
  and procedural changes. This is especially true for
  any changes that require administrative approval or
  funding appropriations.
• Necessary changes in staff  attitude may mean
  personnel changes are needed. If the staff do not
  support the CCP  approach,  the CCP will  require
  additional effort and perhaps  personnel changes to
  be successful.

• Time is required  to identify  and eliminate  any
  additional performance-limiting factors found during
  the CCP.

Since the  goal of implementing  the CCP is to correct
performance-limiting  factors  until  the desired water
quality is achieved,  the details  of the implementation
often will be site-specific and, therefore, should be left
to the individuals implementing the CCP.

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                                             SECTIONS

                                    RESULTS OF CASE STUDIES
Thirteen CPEs were conducted in 1988 and 1989; 11
at conventional drinking  water treatment facilities and
2 at facilities using direct filtration. Of the 13, 9 were
completed in Montana, and 2 each were completed in
Ohio and  Kentucky. The plants  ranged in size from
3.8 to 202 L/s  (86,000-10,000,000 gpd). Table 3-1
summarizes the design  capacity and  type of plants
evaluated. Conventional  plants are defined as  using
flash  mix,  flocculation,  sedimentation,  filtration, and
disinfection unit processes  primarily  for  turbidity
re.voval and disinfection.
Table 3-1. Summary of Plants Where CPEs Have Been
Conducted
Plant No. Design Capacity Process Type
1
2
3
4
5
6
7
8
g
10
11
12
13
7 mgd
3 mgd
5 mgd
60 gpm
3 mgd
4 mgd
10 mgd
250 gpm
650 gpm
350 gpm
300 gpm
500 gpm
1 .5 mgd
Lime Softening'/Conventional
Conventional
Conventional
Conventional
Direct Filtration
Lime Softening'/Conventional
Conventional
Lime Softening7Conventional
Direct Filtration
Conventional
Conventional
Conventional
Conventional
   * Equipped with  reactor ciarifiers combining flocculation and
    sedimentation in one basin.
 CPE Findings

 Nearly all  13 case studies  revealed  significant
 information   about   each   plant's  condition,
 administration,  and operation, including findings that
 had not been identified in previous inspections.

 • At Plant 6, the CPE team discovered that plant staff
   bypassed the reactor clarifier during winter months
   and proceeded  to operate  using  direct filtration
   without any  chemical coagulant aids. This practice
   was discovered  by  thoroughly examining plant
   operating  records  and  conducting  followup
  interviews with the plant staff. While the operating
  records provided only a hint of a problem, the CPE
  team was able to pinpoint the problem by  posing
  directed questions to the staff.

• At Plant 3, a direct discharge of backwash water to
  a stream was identified. This practice violated  the
  State's discharge regulations.

• At  Plant  12, the CPE  team  learned that  the
  dilapidated condition of the  plant prevented  it from
  providing  acceptable  finished  water  to  the
  community. While it originally appeared  that  the
  plant would  not  be able to afford the necessary
  repairs, the  CPE  team's  review  of the  plant's
  operating  budget  and available resources led  the
  community to believe that sufficient funds were in
  fact available to  repair  the plant  and to redirect
  priorities.

The case  studies  also  clearly indicate  that  the
involvement of community administrators is a critical
part of the CPE and, ultimately, to improving a plant's
performance. Administrators frequently had  not been
informed of previous inspection results and potential
or  existing  problems  and,  therefore,  had  not
implemented  remedial  actions.  In a CPE,  the
administrators  are  involved  from the  outset  and
informed of  the evaluation results during the  exit
meeting.  Informing  administrators  of  performance
problems during  this  meeting  often  led  to their
decision to change priorities regarding water treatment
improvements and  policies at the plant. Without the
CPE  results,  existing plant staff frequently were
unable to enlist the support of administrators or to set
priorities for remedial actions.

• At Plant 2, the CPE team discovered that the plant
   operated at its peak rate 24 hr/day during  maximum
   demand seasons. When the team reviewed  data on
   the service population, they learned that per capita
   water use  was  excessive.  By  lowering peak
   demands  to  more  typical  rates, the  plant could
   operate within acceptable loading rates to  achieve
   compliance  with  applicable standards.  When the
   CPE  team  informed administrators  of  this  fact
   during the exit meeting, they decided to change the
   water rate structure and penalize high  consumption.

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    At the same time,  administrators  initiated a leak
    detection survey and identified a major leak into an
    old, abandoned oak  stave pipeline. Together, these
    administrative actions substantially reduced water
    demand  and   enabled  the  plant  to  achieve
    acceptable treated  water  quality without  major
    expenditures.

 •  At Plant  12,  the team  identified severe  finished
    water  quality  problems  (very high finished  water
    turbidity levels)  that  previously went undetected or
    unreported. Mechanical equipment was in a state of
    disrepair, thereby adding to the plant's performance
    problems.  In  addition,  plant administrators had
    scheduled  several  major  extensions  to the
    distribution system; however,  when informed by the
    CPE team of  the  performance problems, the
    administrators intended to redirect their resources
    from the distribution  extensions to upgrading  the
    water treatment plant facilities.

 •  Town administrators  for Plant 13 had signed long-
    term agreements to supply water to a new industry
    and  another water district. Some aspects  of the
    agreement were considered major concessions  to
    attract  the  industry,  which  would employ  500
    people. Rrst,  it was estimated  that  when these
    users came on line they  would represent one third
   of  the plant's  current  capacity,  possibly
   necessitating  facility  modifications  to  provide
   additional plant capacity. In addition, the agreement
   also  required the  town to supply  the  water at a
   lower cost  than  that currently paid by the town's
   own  drinking water customers. When the CPE team
   presented town administrators with this information,
   they indicated that they would consider initiating a
   rate  study  and examine  the  need  to  renegotiate
   these agreements to supply water.

The case studies showed that in all plants but three,
plant performance  was  much worse than previously
reported data had  indicated. In two  cases,  finished
water quality was so poor that the state threatened to
institute a boil  order unless the  facilities immediately
made  improvements. The  CPE teams discovered
these performance problems despite  the  fact that
monthly operating reports usually showed that finished
water quality  met drinking  water  standards.  These
findings indicate that the  present requirement  to
sample  turbidity from the clearwell  on a daily basis
does not  accurately reflect actual finished  water
quality at many plants. The CPE team initiated special
studies  that included developing turbidity vs. time
profiles  on filtered water.

• At Plant 2,  12 months of data  previously submitted
  to the State revealed no violations. However, when
  the CPE team measured turbidity before and after
  the filter backwash and plotted the data (see Figure
  3-1),  they discovered  a turbidity breakthrough  of
  5.8 NTU. Figure 3-1 also reveals that a decision to
    delay  the  backwash  resulted  in  a significant
    increase in  filtered water  turbidity  just  prior to
    initiating the backwash  cycle. Similarly, when the
    CPE team reviewed operating data for a 1-yr period
    at Plant 12,  they learned  that  finished  water
    turbidities  were  very  consistent  and  rarely
    exceeded  1.0  NTU  (see Figure 3-2). However,
    when the  team  measured turbidities during the
    CPE, they discovered clearwell turbidities in excess
    of 6.0 NTU. The data reported to  the State must be
    representative of actual operating  conditions.

 These results  indicate  that  data  from daily grab
 samples may  not reflect  true performance  and  that
 data collected  over shorter time periods (such  as
 hours or  minutes) is necessary. This suggests  that
 facilities should  perform  either in-line  continuous
 turbidity monitoring and  recording on  each  filter, or
 manual  monitoring of each filter effluent on an  hourly
 basis.  Less frequent monitoring would likely  miss
 turbidity spikes.

 The  case studies indicated that plant  operators  and
 administrators generally did not recognize the serious
 public health  impacts  of  short-term  digressions in
 treated water quality. For example, at Plants 2, 4, and
 6,  plant operators and administrators did not  take
 immediate  action  to correct short-term  breakdowns
 even when they were aware of performance problems.

 A key finding  of  the studies is that,  because most
 small water treatment facilities are only operated for 8
 or 12 hr/day, they tend to  have excess capacity. The
 excess capacity results from being able  to operate at
 a lower flow rate for longer periods  of time,  enabling
 many small plants to address unit process limitations.
 For example, Plant 8  operated at its  16-L/s (250-gpm)
 capacity for only several hours each day even  when
 turbidity  levels in the  surface  water  exceeded the
 plant's treatment capability. The  CPE  projected that,
 by  reducing the plant flow to  8 Us (125 gpm) and
 operating for  up  to  12  hr,  the plant  could  treat
 turbidities of any anticipated level. Likewise,  at Plant
 5, reducing the plant flow from 132 L/s  (2,100 gpm) to
 69  L/s  (1,100  gpm)  relieved a  severe  air   binding
 problem   and  enabled  the  plant  to  operate
 successfully. At Plants 8 and 5,  water demands were
 met even with reduced plant flows; however, this may
 not always  be the case.

The case studies revealed that proper control of the
filtration   process  is key  to  improving  plant
performance.

• At  Plant  2,  filter  rate  controllers  malfunctioned
  causing the filter effluent valves to open and close
  every  few seconds. The filter flow rate changed
  from 0 to 63 L/s (1,000 gpm). The filter  effluent
  turbidities also  varied,  indicating  that particles
  previously filtered were washed through the filter to
  the clearwell. While plant staff knew that the valve
                                                  10

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Figure 3-1.   Plant 2 turbidity profile.
             Turbidity, NTU

                6 -r
                5 -
                4 -
                3 -
                2 -
                 1 -
                                                      FILTER BACKWASH
                                  -i	r
                                  100             200             300

                                  MINUTES AFTER START OF SPECIAL STUDY
400
Figure 3-2. Plant 12 finished water turbidity profile.
       1
           in

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           in
                                                                                               Present
                                                                                             Requi rement
                                                                                               Future
                                                                                             Requi rement
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           SEP88 OCT  NOV  DEC JRN89  FEB  MflR   RPR  MRY  JUN  JUL  RUG  SEP   OCT
                                                   11

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   "jumped around,"  they did  not  realize that it
   affected  filter  performance. The studies clearly
   indicate that filter rate controllers must be properly
   maintained to allow the filters to operate correctly.

 • At Plant 2,  when  plant staff removed one filter for
   washing, the entire  plant flow was  directed to the
   remaining filter.  This caused  severe  turbidity
   breakthrough.

 • At Plant  8, filters were  "started  dirty," causing a
   serious detrimental effect on filtered water quality.

 • At Plant 2, operators changed the flow rate without
   adjusting chemical  feed  rates.  This  resulted in
   improper feed  of coagulant  chemicals  and
   subsequent degradation in finished water quality.

 The  case  studies revealed  that all  13  plants
 implemented only limited  process control efforts. Little
 testing  or data  interpretation,  both  of which are
 imperative  to  making  informed operating  decisions,
 were conducted.  As a  result,  improper operating
 practices, such as bumping filters or waiting  too  long
 to backwash filters, were  widespread. For example, at
 Plant 12, water was allowed to drop from the troughs
 onto  the  filter  media,  which  clearly  violates basic
 principles of filter operation.

 CCP Findings

 CCPs were implemented at 2 of  the 13 plants.  The
 objective of the CCP studies was to determine if the
 approach could improve plant performance and enable
 the plants to comply with  the  SWTR without major
 capital improvements.  The specific findings  of the
 CCPs, which were conducted at Plants 1 and 5, are
 also presented in Section  4.

 Implementation of these CCPs  enabled both plants to
 meet the future finished  water turbidity requirements
of the  SWTR  by  implementing  process  control
 programs  and providing  operator training.  The
approach demonstrated the potential for drinking water
treatment  facilities to meet regulatory  requirements
through  improved  operation, maintenance,  and
administration rather than major capital improvements.

• At Plant 5, city administrators originally had  planned
  to  spend approximately  $1  million  to  construct
  sedimentation  basin  facilities  and  related
  improvements. They felt  the major  capital
  improvements were necessary to ensure that the
  plant  could  achieve  compliance  with   the
  forthcoming SWTR turbidity requirements. After the
  CCP was conducted, however, construction of the
  improvements  was  delayed  until  such  time  that
  water demands required that the  plant operate at
  higher rates.  As a result of the  CCP, plant  staff
  developed  increased  confidence   that,  by
  implementing process  controls, the plant could
   produce  excellent  water  quality  despite high  raw
   water turbidities.  The  CCP also  revealed that
   accurate  coagulant doses  could  be selected by
   using the jar test/filter paper procedure.

 • At Plant  1,  the  CCP dramatically improved plant
   performance.  Turbidity removal in the  reactor
   clarifiers was improved and stabilized, and chemical
   requirements were  minimized. The  improvement
   resulted from a combination of process control and
   monitoring,  as well as  several major  process
   adjustments.

 To achieve the  desired  results,  CCPs should  be
 implemented over a period of at least 6 months, since
 time  is  necessary to implement  process  control
 programs, purchase equipment,  provide training, and
 document stable finished water quality for variable raw
 water conditions.  The  case studies demonstrated that
 process control programs improved the performance
 of individual unit processes at the two plants,  thereby
 leading to improved finished water quality.

 Overall Factors Limiting Performance

 A CPE team evaluated 65 performance-limiting factors
 at each of the 13  plants; the top  10  performance-
 limiting  factors are presented  in  Table  3-2.  It is
 important to  remember  that no  one factor was
responsible for limiting plant performance, but rather a
unique  combination  of factors  contributed  to
performance problems.
Table 3-2.
 Rank
           Top Ranking Performance-Limiting  Factors
           Identified at 13 Facilities
              Factor
                           No. Plants    Category
       Operator Application of
       Concepts and Testing to
       Process Control
13
Operations
2
3
4
5
6
7
8
g
10
Process Control Testing
Process Controllability/
Flexibility
Disinfection
Sedimentation
Staff Number
Filtration
Policies
Flocculation
Maintenance
11
13
9
10
7
7
7
6
7
Operations
Design
Design
Design
Administration
Design
Administration
Design
Maintenance
  The highest ranking performance limiting factors fell
  in the operations category, and were related to the
  inability of  plant staff to  respond to water quality
  changes with appropriate chemicals in appropriate
  doses.  In addition,  plant staff  frequently made
  improper operating decisions  because they lacked
  understanding  of  unit  processes and  associated
  controls. Compounding these  problems was a lack
                                                 12

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 of process control testing programs at all but two of
 the plants.

 Design factors represented 5 of the performance
 limiting  factors  in  the  top  10  list.  Process
 controllability and flexibility was the highest ranked
 design  limitation. It  was cited  most  frequently
 because  of  limitations in type  and  location  of
 chemical feed options, and in control aspects such
 as  filter-  regulating valves  or  plant  flow  control
 valves.   The  CPE  team  noted  that  minor
 modifications  could  address these  performance
 limiting factors at the facilities.

 Disinfection  facilities   were  identified  as  a
 performance  limiting factor at 9 plants because  of
 inadequate  detention  time  in  clearwells  or
 transmission lines. The SWTR will require a plant to
 provide a certain CT  value, which is obtained by
 multiplying the disinfectant  concentration by the
 actual  contact time. Most of the  plants  relied  on
 unbaffled clearwells to provide most of the required
 detention  time. These clearwells were projected to
 provide inadequate CT because  of expected severe
 short circuiting.  However,  modifications  to the
 clearwells, such  as  installing  baffles, may  allow
 these plants  to meet  the  CT requirements of the
 SWTR.  Findings  of disinfection inadequacy  were
 based  on the CPE  team's  estimates of the
 allowable  contact time at each  plant.  No thorough
 hydraulic  analyses, as  required  by  the  SWTR,
 could be conducted within  the scope of this project.
 The  identification of  disinfection  inadequacy was
 tentative  and  is  meant as  a  signal  that current
 operation  might  not  be  adequate  to  meet the
 disinfection requirements to be established by each
 State.

 Sedimentation basin design was  identified   as  a
 performance-limiting factor at 10 plants. The impact
 was  periodic  and  seasonal during high turbidity or
 high- demand episodes. The CPE team projected
that  improved operation could minimize the  impact
that the marginal basins had on plant performance
 (for example,  longer run times at lower flow rates or
improved coagulation control).
 • Filters presented problems at 7 of the facilities. The
   CPE team identified  this factor because of  air
   binding (2 plants), backwash  limitations  (2 plants),
   and  possible filter  underdrain  or  support gravel
   problems (three  plants). The team felt that the  air)
   binding  and  backwash  limitations could   be'
   minimized or overcome  by improved operational
   practices, and that the underdrain or support gravel
   damage could  have been avoided if the  operations
   personnel had  better understood the  filtration
   process.  This damage appeared to be caused  by
   introduction of air or  by excessive instantaneous
   hydraulic load at the beginning of a backwash.

• Flocculation  capability  was identified   as
   performance limiting at 6  plants because of limited
   basin volume and  lack of staging.  The CPE team
   concluded that improved operations could minimize
   the  impact of this  factor (for  example, lowering
   hydraulic  loadings, installing  baffles,  modifying
   coagulants).

• Administrative factors  (including  staff  number and
   administrative policies) also were included in the
   top  10 list.  An  inadequate number  of staff  to
   properly run  the facilities was noted  at 7 plants.
   This deficiency was critical considering the need  to
   add a  process control program  and associated
   responsibilities  at these  plants.  Frequently,
   administrators  were unaware  of  operating
   requirements,  or had  set water rates too low  to
   maintain  adequate treatment  or establish a self-
   sustaining utility.  Few administrative personnel
   understood the  severity of short-term excursions
   from high quality treated water.

•  Maintenance factors were identified as impacting 7
   of the plants. Operators who lacked understanding
   of process  operations abandoned  many of the
   automatic and/or  manual  control  systems at the
   plants. The CPE  team identified several facilities
   where maintenance  activities  were  completely
   neglected,  sometimes due  to administrative
   indifference. The  team concluded  that  improved
   understanding  of operations  and  maintenance,
   coupled with an  improved administrative attitude,
   could lead to improved  plant performance.
                                               13

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                                             SECTION 4

                                          CASE HISTORIES

  The following case histories provide a detailed summary of the results from each of the  13 CPEs on which
  this report is based.  Each case history consists  of a facility description, results of the Major Unit Process
  Evaluation and Performance  Assessment,  and  a discussion  of the  factors found limiting the  plant's
  performance. The applicability  of a CCP  is also  discussed  for each  plant as are the results of  the CCPs
  completed at two plants. These CPEs were completed as part of the project to develop and formalize these
  procedures for water treatment plants. Some aspects  of the procedures were refined as more CPEs were
  completed. As the procedures evolved through these refinements, some of the ways in which the results are
  presented have changed. Some inconsistencies between the presentation of the results of the different case
  histories, therefore, may be observed.
 Plant 1

 Facility Description
 Constructed in 1974, Plant 1 is owned and operated
 by the city and serves approximately 10,000 persons,
 with no significant industrial water users. It consists of
 a  pre-sedimentation basin followed by conventional
 treatment and is used  as a softening facility during
 winter months. Average daily flow for  a  12- month
 period was  66 L/s  (1.5 mgd), with an average  daily
 flow during the peak month of 131  L/s (3 mgd). The
 plant includes the following unit processes (see Figure
 4-1):

 •  Three  constant-speed,  raw water pumps:  two 25-
   hp, 126-L/s  (2,000-gpm) and  one  15-hp,  91-L/s
   (1,450-gpm)

 •  8.7 million-L (2.3 mil-gal) earthen pre-sedimentation
   basin

 •  Three  15-hp,  113-L/s (1,800-gpm) constant-speed,
   low-service pumps

•  Chemical addition (alum, lime, and Dycafloc 587-C)

•  Two  17.7-m  x  17.7-m  (58-ft  x 58-ft)  upflow
  clarifiers, 6.4 m (21 ft) and 6.0 m (19.8 ft) deep

•  Recarbonation with liquid carbon dioxide

•  Four 7.6-m x 7.6-m (25-ft x 25-ft) dual media filters

•  1.1 million-L (300,000-gal) clearwell

• Disinfection
 • Fluoridation (sodium silica fluoride)

 • Sludge removal and thickening

 • Sludge drying beds

 • Three high-service pumps:  100, 113,  and 157 L/s
   (1,600, 1,800 and 2,500 gpm)

 The three  raw water pumps transfer water from the
 nearby river through a 61-cm  (24-in) line to  the pre-
 sedimentation basin. The three low-service pumps lift
 the  water from  the  pre-sedimentation  basin
 approximately -18 cm (7 in), so that it  can  flow  by
 gravity through the plant's unit processes.

 Powdered activated  carbon  is added to  the  water in
 the pre-sedimentation basin for  taste and odor control
 and  a cationic polymer is injected following  the raw
 water  pumps. Alum and  lime  are added  in  the
 flocculation  area of the two  22-L/s (500,000-gpd)
 solids contact clarifiers.

 The  clarifiers are square with circular sludge  removal
 mechanisms. Prior to the clarifiers, water from a 14-
 L/s (220- gpm)  "soda well" is  pumped into  the raw"
 water stream.  Hydraulic conditions  cause an uneven
 split  of this softer water between the two clarifiers.

Water flows through the clarifiers  to a recarbonation
 basin, where the pH is lowered, and onto four dual
 media filters. From the filters, the finished water flows
into the clearwell. Chlorine and fluoride are added to
the water  as it; enters the clearwell. The three high-
service pumps deliver finished water to the distribution
system.
                                                  15

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Figure 4-1.  Plant 1 process flow diagram.
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Major Unit Process Evaluation
Figure 4-2  illustrates  the  assessed  capacity  and
projected  performance  of each of the plant's major
unit processes in a performance  potential graph. The
vertical broken lines indicate the  annual average flow
of 70 L/s (1.6 mgd), the peak monthly flow of 131 Us
(3 mgd), and the design capacity of 307 L/s (7 mgd).

As  Figure  4-2 shows,  the  raw  water pumps,  low-
service pumps, filters,  and  high-  service pumps are
rated at  the  307-L/s  (7-mgd)  plant design  flow.
Potential  capacities of  the  pre-sedimentation basin
and the clarifiers are rated at less than design.

The  pre-sedimentation basin was derated because of
short circuiting through  the basin and  no capability to
add coagulant aids. Also, return of backwash water to
the effluent  end  of the  basin results in excessive
turbidity levels in  the raw water. The basin was rated
above the peak monthly flow of the plant.

The clarifier/flocculator was rated at 136 L/s (3.1 mgd)
with  one unit in service and 272  L/s  (6.2 mgd)  with
both  in service.  The corner sweeps on the  sludge
mechanisms have failed allowing  excessive  amounts
of sludge  to  build up in the basin corners. Sloughing
of the sludge coupled with inconsistent weir elevations
has  resulted  in  periodic  solids  loss.  The clari-
flocculators  were derated  because  of  these
conditions.

Performance Assessment
Plant 1 is  currently  required to  produce finished water
with  turbidity levels less than 1.0  NTU and with free
chlorine at levels that will ensure less than 0.2 mg/L at
all points in  the distribution system.  Fluoride  is added
to achieve  a 0.9-1.1  mg/L  residual  in the-finished
water. A  comparison of  plant monitoring data  with
state  requirements  indicated the  plant was operating
in compliance with applicable regulations.  A review of
operating  records,  however,  indicated numerous
excursions   of filter   effluent  turbidities above
acceptable levels.

The  SWTR  will  require  plants to  demonstrate by
regular turbidity  monitoring or  constant recording
turbidimeters, turbidity  at less  than  0.5 NTU greater
than 95 percent of the time. Additionally, theoretical 3-
log removal  and/or inactivation of Giardia cysts and 4-
log removal  and/or inactivation of enteric viruses must
be demonstrated.

Performance-Limiting Factors
The  factors  identified  as having  a major effect on
performance  on  a long-term  repetitive  basis  are
summarized below in order of priority.

1.  Operator Application of  Concepts  and Testing to
    Process  Control -  Operation:  Operation of  the
    plant is  maintenance  rather than process control
    driven. Priorities need to  be established that allow
    process control  to be  integrated into  the daily
    routine of  the  plant staff. This involves  collecting
    additional  process control  data and  interpreting
    the data to direct process  control that  optimizes
    plant performance.

2.  Process Control  Testing - Operation: The lack  of
    process control testing has resulted in incomplete
    data being collected  to determine the  level  of
    plant  performance.  In  addition,  it  is  probably
    masking periods  of  production of poor quality
    finished water. Items of particular concern are lack
    of turbidity testing of raw water and water from the
    clarifiers, and  continuous monitoring of  individual
    filter effluent. Plant data indicate that filter effluent
    "spikes" were  occurring, but it was not possible  to
    determine their severity or duration.

3.  Process Automation - Design: There is a need for
    continuous monitoring and recording turbidimeters
    on the raw water, each filter, and the clearwell.

The factors  identified as having  either a minimal effect
on a long-term repetitive basis  or a major effect on a
periodic basis were prioritized and are summarized
below.

1.  Process Flexibility -  Design:  More  flexibility  is
    necessary in types of  chemicals added and points
    of chemical addition. At the  time of the evaluation,
    alum  and  lime were added to the flocculation
    portion  of the clarifier and polymer was  added
    after  the  low-service pumps.  There   was  no
    process available to feed a filter aid  or flocculent
    aid. Flexibility  to move the alum feed to  a point
    with greater mixing could  reduce  the alum feed
    rate and may  also allow the flocculator  speed  to
    be reduced  to better  optimize  flocculation.  The
    ability to add  a  filter aid  would  improve filter
    performance.

2.  Lack  of Standby  Units -  Design:  There  is no
    standby backwash pump.  If the  existing  pump
    fails, the plant is out  of operation until  it can be
    repaired or replaced.

3.  Preliminary Treatment - Design: Obvious  problems
    exist with  the  pre-sedimentation  basin,  including
    no chemical feed  (except  carbon) to the  basin,
    short  circuiting,^ backwash  water  fouling  of the
    intake  area of  the  low-service  pumps,  and
    difficulty cleaning the pre-sedimentation basin.

4.  Staff Number - Administration: The current major
    emphasis is on maintenance; more time  must be
    spent on process control to improve performance.
    In  addition, the  superintendent  is working  extra
    shifts  to keep the plant operating. At least two
    additional plant operators are necessary for  both
    operations  and  maintenance  activities to  be
    adequately addressed.
                                                   17

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Figure 4-2.  Plant 1 performance potential graph.


    Unit Process
                   Flow, mgd

123456789
                                                                                         10
Raw Water Pumps1
Pro-sedimentation2
Low-service Pumps3
Clari-flocculator"
SOR, gpd/sq ft (1 unit)
SOR, gpd/sq ft (2 units)
Filters*
HLR, gpm/sq ft (1 filters)
HLR, gpm/sq ft (2 filters)
High-service Pumps6







329
154

0.3
0.6










656 9(.
329 4S

0.6 0
1.2 1










i-
32 656 820 984

8 1.1 1.4 1.7 2
5



.0
Annual Avg. Peak Month Design
6/86-6/87 5/86-5/87 Capacity
    1 7.8 mgd with individual pumps - assumes design capacity with continued operation.
    2 Assumes run 2 filters at 2 gpm/sq ft and backwash 2 filters at end of day.
    3 7.8 mgd with individual pumps - assumes design capacity with continued operation.
    * Rated at 800 gpd/sq ft for turbidity removal - use 1,000 gpd/sq ft for softening capacity (weir imbalance).
    s Rated at 2 gpm/sq ft.
    8 2.5 mgd with individual pumps - assumes design capacity with continued operation
5.  Sedimentation -  Design:  The  corners  of the
    clarifiers need to  be grouted to prevent buildup of
    sludge  in the  basins and  the  flow through the
    weirs needs to  be  balanced so  that resulting
    hydraulic gradients do  not  impact the quality  of
    the water from the clarifiers. The combination  of
    un-level  weirs  and  sludge   accumulation in the
    basin corners has led to periodic solids loss in the
    effluent, which severally  degrades  plant
    performance.

6.  Disinfection  - Design: Short circuiting of finished
    water through the clean/veil  results  in inadequate
    contact time for proper disinfection. This problem
    will be amplified with colder  water and higher pHs.

7.  Return Process Streams: Return of the backwash
    water to the pre-sedimentation basin near the low-
    service  pumps'  suction  negatively  impacts  raw
    water quality.

In  addition  to  the  above  major  factors  limiting
performance, other factors were noted  during the
                 evaluation as  having  a minor effect on performance.
                 Action  taken  to  address  these  factors  may  not
                 noticeably improve  plant  performance,  but  may
                 improve the efficiency of plant operation:

                 • The  pre-sedimentation basin  is  not designed to
                   handle high turbidities caused by  runoff  and ice
                   jams.

                 • Flash mixing of chemicals appears inadequate

                 • The  ability  to sample the sludge  return  and the
                   sludge concentration  within  the  clarifiers (top to
                   bottom) is inadequate.

                 Projected Impact of a CCP
                 The  CPE indicated  that  operator training  through  a
                 CCP  would  be  beneficial  for  improving process
                 stability and finished water.

                 CCP Results
                 A CCP was  initiated. Monitoring of the two  reactor
                 clarifiers during the CPE  phase had revealed problems
                                                    18

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 Figure 4-3.   Settled water turbidities from the reactor clarifiers at Plant 1.


               Turbidity, NTU

                   12

                   11

                   10

                    9

                    8

                    7

                    6

                    5

                    4

                    3

                    2

                    1

                    0
14-Mqy-89
         28-ttoy-89


                 Q   BASIN #2
                                                           09-Jul-89           0$-Aug-89
                                                  25-Jun-89           23-Jul-89

                                                   ' +  BASIN #1
with clarifier solids  control.  Thus,  the  CCP efforts
began by expanding process  control in the clarifiers.
Each clarifier was taken out of service so that several
feet of anaerobic lime sludge that had accumulated in
the basins could be removed.

Figure 4-3 shows the finished water turbidity from the
two clarifiers from the time the cleaning operation was
completed in  May  until  the  CCP was concluded in
August. The basins' settled water turbidities gradually
improved  and stabilized  at 1  to 2  NTU;  both basins
exhibited  equal   performance.   Activities   that
contributed  to  this consistent performance included
controlled flow splitting, equalized  chemical doses to
each basin,  and  shutting  off of  a  well  that  was
contributing  a disproportionate amount of flow to basin
2. The reactor  clarifiers  achieved  this  performance
despite variable influent turbidities to the  basins from
the pre-sedimentation pond, as shown in Figure 4-4.

Most importantly,  the  improved  reactor  clarifier
performance  "carried  over"  to  improve  the
consistency of turbidity removal by the filters. Figure
4-5 shows the overall plant finished water turbidity,
which stabilized at  less than 0.2 NTU  since the end of
June 1989,  coinciding with stable performance  from
the contact  clarifiers. The improved performance  was
achieved despite an increase in treated water  volume
                                 and  a gradual increase in  turbidities from the  pre-
                                 sedimentation basin during the last month of the CCP.

                                 The  CCP resulted in dramatic improvement of plant
                                 performance  without  major  capital improvements.
                                 Process control and monitoring activities, coupled with
                                 several  major process adjustments, improved  and
                                 stabilized turbidity removal in the reactor clarifiers.
                                                   19

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Figure 4-4.   Effluent turbidity from the presedimentation pond for Plant 1.
                Turbidity,
                    100
NTU
                       14-!
Mqy-8911-Jun-89I     09-Jul-89T    06-Aug-S9
       28-Hay-89           25-Jun-89           23-Jul-89
Figure 4-5.   Finished water turbidity profile from Plant 1.
             Turbidity, NTU
                  .8
                  .7
                  .6
                  .5
                  .4
                  .3
                  .2
                 1.1
                   1
                 0.9
                 0.8
                 0.7
                 0.6
                 0.5
                 0.4
                 0.3
                 0.2
                 0.1
                                     Future Requirement
                    14-May-89           11-Jun-89            09-Jul-89     |     06-Aug-89
                               28-May-89            25-Jun-89            23-Jul-89
                                                      20

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 Plant 2

 Facility Description
 Plant  2,  constructed in 1931 and expanded  and
 upgraded in 1976,  has  approximately  1,000 service
 connections and no significant industrial water users.
 It consists of  a conventional  treatment  process
 including  flash  mix,  flocculation,  sedimentation,  and
 filtration, and  no pre-sedimentation. Source  water is
 provided by the  nearby river.

 Plant records  for a 12-month period show daily water
 production to  be  1.1-6.1 million L  (0.3-1.6  mil gal).
 Flow records  are obtained from  the plant  finished
 water  meter and do  not include water  used  for filter
 backwash. During the CPE,  water  was produced over
 an 8-hr day at an effluent flow rate of about 89 L/s (2
 mgd);  peak effluent  flow was  131  L/s (3 mgd). Plant
 influent flow is not measured  because the raw water
 meter  is inoperable.  Plant 2 includes the following unit
 processes (see Figure 4-6):

 • Two vertical turbine raw water  pumps rated at 76
  and 69 L/s  (1,200 and  1,100 gpm), and one 28-L/s
  (450-gpm) engine driven raw water pump

 • Chemical addition of alum,  polymer,  and lime with
  in-line mechanical flash mix for the alum

 • Two 206,430-L (54,540-gal) parallel flocculation
  basins  with  two variable speed  turbine mixtures in
  parallel

 • Two 666,160-L (176,000-gal) sedimentation basins
  with tube settlers over half their surface area

 • Three  3.4-m  x  4.9-m (11-ft x 16-ft) mixed media
  filters with Leopold underdrains

 • Gas chlorination system

 • 204,390-L (50,400-gal) clearwell

 • Two centrifugal high-service pumps rated at 72 and
  94 L/s  (1,150 and 1,500 gpm), and one  standby
  natural gas driven vertical turbine pump rated at 27
  L/s (425 gpm)

 Water  flows by gravity to a wet well through  either a
 shallow culvert near the bank of the river or through a
 second pipe extending toward  the  center of the river
at an  unknown  distance and  depth.  The  vertical
turbine pumps deliver water to the  plant from  the wet
well. The turbine pump supplies  water  from  the
surface intake. A float control in the clearwell initiates
the raw water pumps.

Alum is added to the raw water  prior to  an in-line
mechanical  rapid mixer; lime and polymer are added
downstream of  the  mixer prior to  the  flocculation
basins. Chemical addition is  not flow paced, although
 the  influent flow varies because raw water pumps are
 initiated and  terminated several times a day.  After
 chemical addition,  the water  flows  to  two  parallel
 flocculation basins with two parallel- operating variable
 speed turbine flocculators. Subsequently,  water  flows
 to  two  sedimentation basins  equipped  with  tube
 settlers. During the evaluation, flow did  not  appear
 evenly     split     between     the     two
 flocculation/sedimentation treatment trains, and the
 clarifier weirs were uneven.

 Sludge is  manually  removed from  the sedimentation
 basins  approximately  once  a  year.Following
 sedimentation, the water flows through a weir to  three
 mixed  media filters with  Leopold underdrains.
 Powdered  activated  carbon is  added once a day to
 the  water  prior to  filtration.   Filtration  rates are
 automatically adjusted by filter  water level floats that
 control  the filter  effluent  valves. At the time of the
 evaluation, one filter  was out of service because  of an
 inoperable effluent control valve. Another filter effluent
 control  valve was malfunctioning and was observed to
 readjust the flow rate by  over 69  L/s (1,100  gpm)
 repeatedly within a few minutes.

 The filters  are normally backwashed once a day; the
 process is  initiated manually but at automatically timed
 intervals and includes surface washing. The backwash
 rate can be set as high as 189 Us (3,000 gpm).

 Filtered water is disinfected with chlorine and is stored
 in the clearwell. The three high-service pumps deliver
 the water to the distribution system.

 Spent  filter backwash water flows  by gravity  to  a
 sedimentation basin,  which overflows to the raw water
 wet well. Each backwash sedimentation basin has the
 capacity for one backwash before  excessive solids
 overflow the effluent  weirs and return to the raw water
 wet  well. The backwash sedimentation  basins are
 normally cleaned once a year.

 Sludge  from the flocculation,  sedimentation basins,
 and  backwash water sedimentation  basins are
 pumped to two sand  drying beds. The dried sludge is
 disposed of at the landfill.

 Major Unit Process  Evaluation
 The performance potential graph is shown in Figure 4-
 7. The flows listed across the top of the graph are the
 maximum  at  which  the  plant can  operate while
 remaining in compliance with applicable regulations.
 Neither  the raw water  pumps  nor  the  high-service
 pumps  were rated  because  the condition of the
 impellers and the actual pump output were not known.

The flash mix was rated at 131  L/s  (3 mgd), where it
can produce a G  value of approximately 3,000 sec-1.
The  in-line mechanical  mixer  would probably be
limited  by  water velocity in the pipeline rather  than
mixing capability.
                                                  21

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Figure 4-6.  Plant 2 process flow diagram.
                                   -ซ  6
                                 .llrf
                                              22

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Figure 4-7.  Plant 2 performance potential graph.
    Unit Process
                     Flow, mqd
                        2
    Raw-water Pumps


    Flash Mix


    Flocculation1
      Detention time, min


    Sedimentation2
      SOR, gpd/sq ft


    Filtration?
      HLR, gpm/sq ft


    Disinfection
      Chlorination



    Contact Time4


    High-service Pumps
                                     Not Rated
       78
      1,287
       1.3
Not Rated
                        26
                                                         Present Plant
                                                           Max. Flow
                                        Design
                                         Flow
   1 Rated at 45 min because of single stage.
   2 Rated at 2,000 gpd/sq ft - may be able to use process control to increase capacity. Also rated on summer water quality, but may be
    able to direct filter in winter.
   3 Rated at 4 gpm/sq ft - media and underdrain integrity, need to be verified to justify this rating.
   4 Based on 2-hr detention time
The flocculation basins  were  rated  below the  plant
design flow at 77 L/s (1.75  mgd) for a detention time
of 45  minutes, because  the flocculation basins are
single-stage units.  Altering the  basins  to  provide
multiple-stage  flocculation would  better  control  floe
formation and  justify increasing the basin capacity  to
153 L/s (3.5 mgd).

The sedimentation basins were rated  at 66  L/s  (1.5
mgd),  which results  in a  surface  overflow  rate of 81
m3/m2/d (2,000 gpd/sq ft)  (based on tube  settler area).
However,  improved  flocculation and process control
could increase this rating. Direct filtration might be an
option during  winter months, which would decrease
reliance  on  the sedimentation  basins for solids
settling.

The mixed media filters were rated at 131 L/s (3  mgd)
for a loading rate of 234  m3/m2/d (4 gpm/sq  ft). With
                   precise  process  control,  the filters could  operate
                   successfully at  up to  293  m3/m2/d  (5 gpm/sq  ft);
                   however, the media and underdrain integrity  must be
                   verified  to justify either  rate.  If further  evaluation
                   indicates damage to  the  filter underdrain  or support
                   gravel, the  filters would  be a  major  performance-
                   limiting factor.

                   The disinfection system was rated as two  processes:
                   chlorination  capacity  and  contact  time.  The
                   Chlorination capacity  rating of  131  L/s (3  mgd)
                   indicates that the capacity of the feed unit is sufficient.
                   The contact time, however,  was rated at only 26  L/s
                   (0.6 mgd), the maximum flow through the plant that
                   would provide the recommended  2-hr detention time.
                   The limited  detention time provided at  normal plant
                   flows  compounds  the  importance  of  effective
                   performance of the other treatment processes for  the
                   removal of pathogens.
                                                     23

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In summary, the performance potential graph indicates
the plant should be operated at less than 66 Us (1.5
mgd) during periods of high raw water turbidity. Flow
rates above 66 Us (1.5 mgd) may  be possible without
adversely affecting finished  water quality;  however,
filter run times will probably be significantly  reduced
because of excessive solids loading, thereby reducing
total plant capacity to 66 Us (1.5 mgd).

During winter months,  if  raw  water turbidities  allow
effective direct or in-line direct filtration, plant capacity
may be able to increase to between 66  and 131 Us
(1.5 and  3.0  mgd), depending on whether  or not
flocculation is required for successful operation.

Performance Assessment
A review of the finished water quality monitoring data
indicated the plant has  been operating in compliance
with the current turbidity Maximum Contaminant Level
(MCL) of less  than 1.0 NTU  on a monthly average.
The plant  has, however,  had  periodic  excursions
above 1.0 NTU. The monitoring data also  indicate the
plant may have difficulty meeting the SWTR turbidity
maximum of 0.5 NTU for 95 percent of  the time (as
measured every 4 hr of water production). Figures 4-
8, 4-9, and 4-11  show effluent turbidities obtained
through special studies. Figures 4-10 and 4-12 show
turbidities from  plant data.

Investigation of  the filter media in  the out-of-service
filter bed revealed that  the media  was clean with no
evidence  of  mudball formation. However,  the
evaluation team discovered numerous depressions of
up to 10 cm (4 in) in the surface of the media, and by
probing the filters  found that  support   gravel  had
migrated and mounded. The operators mentioned that
sand, anthracite, and garnet had been removed from
the  clean/veil during cleaning.  Measurement  of the
media pile that had been removed from the clearwell
indicated that approximately 0.2 m3 (7 cu ft) of filter
media had passed  through  the support  gravel. The
migration  of the support gravel, depressions in the
surface of the filter bed, and the passing of 0.2 m3 (7
cu ft) of media through the filter all indicate serious
damage  to the filter  support gravel  and  media.
Typically,  this  type of  damage occurs  when  air is
introduced into the backwash water.

Performance-Limiting Factors
The factors identified  as  having a  major effect on
performance on a long-term repetitive basis  are
summarized below in order of priority.

1.  Operator Application of Concepts -  Operation:
    Process control is needed so  that operators
    respond directly to raw water quality  changes. At
    the time of the evaluation, finished water quality
    was  fluctuating  drastically  with  periods  of  poor
    finished  water production.  Figures 4-8 through 4-
    11 show actual plant data indicating the variability
    in  water  quality and the  extremely   poor  water
    produced, evidenced by the filtered water turbidity
    of 46  NTU from Filter 3  when Filter  1  was
    backwashed (figues 4-8 and 4-9). Plant operations
    staff need  to  vary coagulant and flocculant
    dosages  and to  change plant water flow rates
    when backwashing filters in response  to raw water
    of variable quality.

2.  Process  Control Testing - Operation: Testing to
    monitor the treatment  process is inadequate to
    detect  problem  areas  and  indicate necessary
    adjustments. This lack of testing allows periods of
    extremely  poor water  to  go  undetected  and
    unconnected as shown  in  Figure  4-12.  At  a
    minimum,  additional  jar testing  and  turbidity
    measurements  of  the  raw water, sedimentation
    basin effluent, and  filter effluent will be required to
    indicate appropriate plant chemical dosages  and
    flow rate  adjustments.

3.  Maintenance: Preventive maintenance is lacking at
    the plant. The plant equipment is maintained on a
    crisis basis and  plant  performance is  directly
    compromised. Major treatment  components were
    out  of  service  during  the  evaluation and have
    evidently not been repaired  for  up  to  several
    years. Examples of equipment in need of repair or
    out of service include the raw  water meter,  filter
    effluent control valves, raw water pump, and alum
    feeder flocculator paddles.

4.  Staff Number  - Administration:  The  present
    staffing level does  not allow the water plant to be
    adequately  operated or maintained. A minimum of
    two  additional  staff members are  needed  to
    sufficiently  cover the utility needs. With adequate
    staff, one operator could focus on plant  process
    control  and other utility  employees could
    specialize in either water or wastewater treatment.
5.  Familiarity with Plant Needs - Administration: Plant
    administration needs to become more familiar with
    the  requirements   of  the  plant.  Better
    understanding of the plant's requirements would
    help  garner the administrative  support necessary
    to operate and maintain the plant properly.

6.  Filtration  -  Design: A  limited  evaluation  of  the
    filters revealed potentially serious problems in the
    support  gravel.  Depending on  the outcome  of a
    subsequent detailed evaluation of filter integrity,
    the filters may be  found adequate to 131 Us (3
    mgd). However,  if the  filters are found deficient,
    they  would probably have to be  repaired before
    the  plant could  produce consistent  high quality
    finished water on a continuous basis.

Factors identified as  having either a minimal effect on
a routine basis, or a major effect on a periodic basis
are summarized below.

1.  Pay - Administration: The extremely low pay scale
    and  lack of employee  incentives will  make  it
                                                  24

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Figure 4-8.   Filter 3 turbidity profile, June 8,1988 - Plant 2.
Turbidity, MTU
   6   -

   5   -



   3   -

   2   -
                                                                            46.0
     Noon
1:00
2:00
   3:00
Time of Day
                                                                               4:00
                                                                                      Filter #1
                                                                                     Backwash
                                                                                          Clearwell
         Current Regulatory Maximum - 1.0 NTU
               Proposed Regulatory Maximum - 0.5 NTU
                                                                                                                    6:00
Figure 4-9.   Filter 1 turbidity profile, June 8,1988 - Plant 2.

 Turbidity, NTU
   6   i-
          Current Regulatory Maximum -1.0 NTU
               Proposed Regulatory Maximum - 0.5 NTU
                                                                              Filter #1
                                                                             Backwash
                                                                 Desired Operating - 0.1 NTU
                                                                                                                  Clearwell
       11:00
                     12:00
                                     1:00
                              2:00             3:00
                                   Time of Day
                                                                                     4:00
                                                                                                      500
                                                                                                                     6:00
                                                             25

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Figure 4-10.  Plant 2 performance.
     Turbidity, NTU
        1.2  r-
        1.0
        0.8
        0.6
        0.4
        0.2
                                    Future Regulatory Maximum =  0.5 NTU
                                                        I
                                                                       I
                                         10
                                                       15             20
                                                             Days
                                                                       2.0
                                                                          Desired Operating =  0.1 NTU
                                                                         I              I              I
                                                                        25
                                                                                      30
                                                                                                    35
Figure 4-11.  Filter effluent turbidities profile, June 8,1988 - Plant 2.
    Turbidity,
      0.5


      0.4


      0.3


      0.2


      0.1
NTU
                    Future Regulatory Maximum = 0.5 NTU
       Filter #3  ~
                                                                         Desired Operating =  0.1 NTU
                                                    I
                                                            I
                                                    4                   6
                                                             Minutes
                                                                                                    10
                                                             26

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Figure 4-12. Plant 2 performance - May 1988.
    Turbidity, NTU

      1.2 i-
      1.0
      0.8
      0.6
      0.4
      0.2
                         1.6  1.6
                                           Future Regulatory Maximum = 0.5 NT
                                                                            Desired Operating = 0.1 NTU
                                      10
                                                     15

                                                    Days
                                                                   20
                                                                                 25
                                          30
    difficult to retain  present employees and to attract
    additional qualified help.

2.  Turbidity/Pre-sedimentation - Design:  Excessive
    turbidity levels  during  portions  of the  year and
    fluctuations  during  high  demand periods  have
    degraded effluent quality.  Pre-sedimentation would
    minimize turbidity fluctuations and result in a more
    consistent  raw water  quality.  Continuing
    operations without a pre-sedimentation basin may
    require  reducing plant flow  rates  during  high
    turbidity periods.

3.  Sedimentation - Design: Surface overflow  rates at
    flows  above 66 L/s (1.5 mgd)  may not  allow
    adequate settling of the sludge.  Poor settling can
  •  cause excessive solids loading to the filters and
    subsequently degrade  filter  efficiency.  Uneven
    overflow  weirs  also cause  poor  distribution  of
    water within the  sedimentation  basin,  further
    impairing settling. Manual  sludge removal  twice a
    year  may be   inadequate  to prevent  solids
    carryover  from  the  sedimentation  basins.  This
    practice is also operator intensive.

4.  Hydraulic Loading -  Design: Fluctuations in plant
    flows due to cycling  of constant-speed, raw water
    pumps  during  high  demand  periods  require
    additional  operator  attention to  maintain finished
    water quality. An influent  flow control valve would
    allow plant flow  rates  to be adjusted more
    gradually and set at various rates.

5.  Disinfection  -  Design:  The  lack  of a  standby
    chlorinator, mixing, proportional feed  capability,
    contact  time,  and  automatic  switchover could
    result in inadequate  disinfection on a  periodic
    basis.

6.  Process  Automation  -  Design:   Effluent
    turbidimeters with recorders on each filter effluent
    would be beneficial  to monitor  water  quality.
    Without  such continuous monitoring, an  operator
    would have to take frequent  measurements (i.e.,
    hourly) to monitor plant performance.

7.  Chemical  Feed  -  Design: The carbon feeder
    should be returned to service to replace manual
    addition. The capability to add two polymers would
    be desirable,  with  additional flexibility in chemical
    feed points. A backup alum  feeder is also needed.

8.  Flocculation  Basins  -  Design:  The single-stage
    flocculation basin  makes  control of proper  floe
    formation difficult. The retention time is adequate
    and  minor modifications   may  allow  two-stage
    operation with variable energy input in each stage.

9.  Process Controllability - Design: Chemical feeders
    should be  flow  paced  or  manually adjusted  to
                                                   27

-------
    complement  and  control raw water quality
    changes.

10. Standby Units - Design: No  standby  units  are
    available  for  critical  process  components,
    including backwash  pump,  alum  feeder, and
    chlorinator.

11. Working Conditions - Administration: Conditions at
    the  water  plant discourage staff from  spending
    time at the plant and encourage neglect. Provision
    of a comfortable climate controlled working area
    would  improve operator morale.

In addition  to the above  major  factors limiting
performance, other factors were  noted  during  the
evaluation  as having a minor effect. Action taken to
address these factors  may  not  noticeably improve
plant performance, but may improve efficiency in plant
operation:

•  Preliminary treatment: Grit in the raw water wet well
   and  the lack  of screens on  the intake  piping
   produce operational  problems because of silt and
   debris accumulation.

•  Flow proportioning to units: Raw water flow to the
   sedimentation basins was  not evenly proportioned.
   Operators can control the distribution of flow to the
   units by frequently adjusting valves located in  the
   sedimentation basin influent piping.
Projected Impact of a CCP
Results of the  CPE indicate  performance to be
severely limited by a number of administrative, design,
maintenance, and operations factors. Every major unit
process  was  identified as a  performance-limiting
factor. The evaluation team reached a consensus that
significant improvements in  water  quality could likely
be  achieved  with  a  CCP,  but that  major capital
expenditures may also be  required for the plant  to
meet the proposed finished water quality criteria.

Many of the unit process limitations described in the
performance potential graph could  be eliminated if the
plant were to be operated at a lower capacity than the
present summer water  demand,  which  appears
excessive. Water conservation measures and lowered
water  demands  together  with a  CCP were
recommended.
                                                 28

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Plant 3

Facility Description
Plant  3 is  owned  and  operated  by the city.
Constructed in  1950 and expanded and  upgraded in
1975  and  1976,  it currently  serves  approximately
5,000 people with no significant industrial  water users.
The  plant  uses a  conventional  treatment process
consisting of flash  mix,  flocculation,  sedimentation,
and filtration.

Plant  records for a  12-month period  indicate that the
average amount of water  treated daily  was  41  L/s
(0.94  mgd), with a minimum of 22 L/s (0.5 mgd) and a
maximum  of 114 Us  (2.6 mgd).  These daily flows
were pumped through the plant in less than 24 hr  and
therefore do not indicate the  operational capacity of
the plant. It is typically  operated at three  standard
rates  -  69,  101, or 202  L/s  (1,100,  1,600,  or 3,200
gpm)  - for  less  than 24  hr.  Plant 3 includes  the
following unit processes (see Figure 4-13):

•  Three vertical turbine raw water pumps: two 25-hp,
   110-L/s (1,750-gpm) and one 15-hp, 63-L/s  (1,000-
   gpm)

•  Chemical addition (alum and polymer) with an in-
   line mixer

•  302,800-L (80,000-gal) flocculation  basin  with  a
   variable speed vertical mixing unit

•  Two sedimentation basins (each 4.1 m x 18.3 m,
   3.7-m deep [13.5 ft x 60 ft, 12-ft deep])

•  Three mixed media rapid sand filters with Leopold
   underdrains

•  Gas chlorination system

•  246,000-L (65,000-gal) clearwell

•  Four vertical turbine finished-water  pumps:  two
   200-hp,  94-L/s  (1,500-gpm), one  100-hp,  38-L/s
   (600-gpm), and one 50-hp, 22-L/s (350 gpm)

Raw water flows by gravity through three 46-cm  (18-
in) diameter perforated  pipes located beneath  the
source creek into a raw water wet well. The three raw
water pumps deliver  water from the wet well to the
flocculation basin.

Alum and polymer are added  to the flow prior to the
flash  mix. The plant's in-line  mechanical flash mixer
was not in use at the time of the site visit because of
maintenance problems; therefore, the only chemical
mixing was caused  by turbulence in the line at nearby
elbows.

After chemical addition,  the  water  flows  into  the
single-stage flocculation  basin with a  variable speed
vertical mixing unit that supplies up to a G value of 70
sec-1.  Following flocculation, the  water flows  by
gravity into two parallel sedimentation basins equipped
with tube settlers. During the evaluation, the flow was
not evenly split between the two sedimentation basins.

Following  sedimentation,  the water  flows to three
mixed  media  filters  with  Leopold  underdrains. The
filters appeared to  be in good  con.dition, but some
chemical residue had accumulated  on the anthracite.
These filters are typically  washed  at  about  189  L/s
(3,800 gpm), which corresponds to 972 m3/m2/d (16.6
gpm/sq ft). Washing typically  occurs at the end of  the
day so that  the filters  start clean the  following
morning.

The filtered water is disinfected with chlorine, then
flows into the clearwell,  where the four high-service
pumps are available.

Sludge from the sedimentation basins and backwash
water from the filters are directed to two  earthen
sludge settling ponds. At the time  of  the  evaluation,
the plant was  discharging overflow from the ponds to
the creek  without  a  National  Pollutant  Discharge
Elimination System (NPDES)  permit.

Major Unit Process Evaluation
The performance potential graph is shown in Figure 4-
14. As Figure 4-14 shows, the potential capacities of
the raw water pumps, high-service  pumps, and filters
were  rated  at the 219-L/s  (5-mgd)  plant design flow.
The flocculation basin, sedimentation  basins, and  the
disinfection  system  were  rated  at  less  than plant
design flow. The single-stage flocculation basin was
derated because control  of  floe formation  is more
difficult with a single-stage than  with  a multiple-stage
flocculation  system.  The sedimentation  basins   are
limited by  a high surface overflow rate,  which  can
allow solids to  be carried over to the  filters. The
disinfection  system was not  considered  adequate at
flow rates  above 166  L/s  (3.8  mgd), because  the
clearwell and  transmission  lines provide  inadequate
detention times at these rates.

The sludge settling  ponds were not rated but were
determined  inadequate at current  flows,  unless  the
plant  obtains an NPDES permit to allow  discharge to
the creek.  Without operational changes such as more
frequent cleaning of the ponds, the effluent quality in
the ponds  may not meet typical  permit requirements
(i.e.,  30  mg/L total  suspended  solids and 1.0  mg/L
total dissolved aluminum).

Figure  4-14  indicates that the  plant  should  be
operated at less  than 101  L/s (2.3 mgd),  if possible.
Short  periods  of  increased  flow  may  be  possible
without adversely affecting  finished  water  quality;
however,  filter run times  will probably  be  reduced
because of excessive solids loading.  The plant may
be operated more hours at the  101 L/s  (1,600 gpm)
                                                   29

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Figure 4-13.  Process flow diagram of Plant 3.
                                        Flash Mix Unit (Not in Service)
^


*


^v

s^~~ ^
\ 3 Mixed Media Filters
                              Clearwell
                                                   -o
                                                         4 High Service Pumps
                                                                                                          3 Raw Water Pumps
                                                   -o
Sludge
Settling
Ponds
                                                             30

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Figure 4-14. Plant 3 performance potential graph.


    Unit Process
                     Flow, mad
                   2          3
    Raw-water Pumps1

    Flash Mix2

    Flocculation3
      Detention time, min


    Sedimentation4
      SOR, gpd/sq ft



    Filiations
      HLR, gpm/sq ft


    Disinfections
      Contact time, min



    High-service Pumps


    Sludge Settling Ponds
      1  5
      926
Not Rated
                  58
         1,852
       72
                  36
- Inadequate at present flow
                              24
                                    Current Annual
                                      Avg. Flow
                    Present Daily7
                      Max. Flow
                                             Design
                                              Flow
   1 Peak flow that plant can treat at worst water quality.
   2 Out of service.
   3 Based on detention time of 45 min and single stage.
   4 Based on 2,000 gpd/sq ft.
   5 Based on 5 gpm/sq ft.
   6 Based on allowing 2 min of contact time in clwarwell and 18 min of contact time in 2,500 ft Of 18-in transmissin line.
   7 Not based on 24 hr/day, so actual flows are higher
 rate  to   overcome  the  limitation   of  the
 flocculation/sedimentation basins.  Also, when  raw
 water turbidities are low the plant may be operated in
 a direct filtration mode, which eliminates the need for
 sedimentation.

 Performance Assessment
 The  city  is  currently required to  produce finished
 water with turbidity  levels less than 1.0 NTU on  a
 monthly average and with free  chlorine at levels that
 will ensure a chlorine residual in excess of 0.2 mg/L at
 all points  in the  distribution  system. A review  of
 monitoring data indicated that the plant was operating
 in compliance with the applicable regulations.

 In  the SWTR, the minimum  requirements for finished
 water turbidity  are much  more  stringent.  Plants need
 to produce finished water with a turbidity less than 0.5
                    NTU more than 95 percent of the time, as measured
                    by regular  daily  monitoring  or constant recording
                    turbidimeters.  Additionally,  the  plant needs  to
                    demonstrate  theoretical  3-log   removal  and/or
                    inactivation of Giardia cysts and 4-log removal and/or
                    inactivation of enteric viruses.  In order to meet these
                    regulations,  surface water  treatment  plants  need  to
                    optimize  process  controls  to  minimize  or  eliminate
                    "spikes"  of  turbidity in the finished water at critical
                    times, such as immediately after backwash.

                    Performance-Limiting Factors
                    The following factor was identified as having  a major
                    effect on performance on a  long-term repetitive basis.

                    1.   Sludge Treatment - Unit Design  Adequacy:  The
                        sludge holding  ponds are currently discharging to
                        the creek, but the plant has no permit to allow this
                                                      31

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    discharge. A letter from the Permits Section of the
    Water Quality Bureau states that  the plant must
    apply  for a  permit, which will  require  certain
    effluent limitations. Permit limitations may require
    major modifications to the plant. Failure to obtain a
    permit and to meet permit  limitations could result
    in sizeable fines being levied against the  town.

Factors identified as  having either a minimal effect on
a routine  basis,  or a major effect on a periodic basis
were prioritized and are summarized below.

1.  Sedimentation  - Unit Design Adequacy: The
    surface  overflow  rate  and  weirs  limit  the
    performance  of  the  sedimentation basin.  If the
    plant were operated at a rate in excess of 101  Us
    (2.3 mgd), the resulting high surface overflow rate
    would  not allow  for adequate  settling. Excessive
    solids would be carried over to the filters, thereby
    degrading filtration performance.

2.  Flocculation  - Unit Design Adequacy:  The single-
    stage  flocculation basin  makes control  of proper
    floe formation  difficult.  Controlling  plant flows at
    rates  below  101  Us  (1,600 gpm)  may  allow
    additional detention time to compensate for the
    lack of a multiple-stage unit.

3.  Lack of Standby  Units- Unit  Design Adequacy:
    There are no standby units for adding chlorine or
    alum.  Failure of either of these chemical feeders
    would  result  in  unacceptable  finished  water
    quality, which may require the plant to shut  down.
    In addition,  there is no  spare backwash pump,
    although, in an emergency, the distribution system
    could provide limited backwash.

4.  Application  of  Concepts  and Testing  to Process
    Control - Operation: The  plant  performance could
    be improved during  periods of variable raw water
    quality by  application of  a thorough  process
    control program.  For example, more frequent  jar
    testing would  provide  data on  which  to  base
    chemical feed points. By  monitoring turbidity from
    the sedimentation basins  several times each day,
    chemical doses  could  be  adjusted to  optimize
    sedimentation basin performance.

    It would  also  be good  practice to monitor  the
    turbidity of water from each of the filters. At the
    present time,  a  daily  turbidity  value  is  being
    recorded for water  from  the clearwell.  This
    measurement may mask higher turbidities coming
    out of the filters.  Significant breakthrough may  be
    occurring that would  not  be  detected by  the
    present monitoring practice.  With continuous
    monitoring and recording  of the turbidity of each
    filter effluent, the increase in  turbidity  following
    backwash could be observed along with the length
    of time the elevated turbidity occurs. This would
    indicate  whether or  not  chemical addition has
    been optimized.

    The use of the flash mix unit, especially during the
    times of the  year  when  direct filtration  can be
    utilized,  would probably  reduce chemical  usage.
    Also, additional  experimentation  with  polymer
    products could result in  the selection  of more
    effective coagulant/flocculent aids.

5.  Policies  -  Administration: Administrative  policy
    limits the frequency  with which  the raw water
    intake can be  backwashed. As a result, the intake
    pipes can accumulate a significant amount of silt
    before backwashing,  thus  reducing  the plant's
    intake  capability. More  frequent backwashing
    would eliminate these periodic limitations  in raw
    water supply.

6.  Chemical Feed Facilities - Unit Design Adequacy.
    Inability  to  feed a filter aid and/or flocculant aid
    could result  in poor  plant performance  during
    periods of variable raw water quality.

7.  Alternate Power - Unit Design Adequacy: There is
    no  standby   power  capability   at  the  plant.
    Therefore,  water would not be supplied  to the
    distribution system during a power outage.

8.  Hydraulic - Unit  Design   Adequacy: Low stream
    flows and upstream  water use  have resulted  in
    periods  when   no raw water  is available  to be
    pumped  into   the plant.   Studies  are  presently
    underway to incorporate in-stream or off- stream
    storage to alleviate this problem.

In addition to the  major factors limiting performance
discussed above,   other  minor  performance-limiting
factors were  noted during the  evaluation. Action taken
to address these factors  may not noticeably improve
plant performance, but may improve efficiency in plant
operation:

•   The  lack of  adequate disinfection  could be  a
    problem when operating the plant  above 166 Us
    (3.8  mgd)  because   of the  potential for short
    circuiting of the clearwell and the limited detention
    time provided in the transmission mains.

•   The lack  of   automatic  continuous  turbidity
    monitoring and recording on the raw and finished
    water from each filter  requires the operations  staff
    to obtain this  information  manually on a periodic
    basis. Not only does this require an additional time
    commitment from the operators, but  periodic
    information  is  not as  effective as a continuous
    record.

•   The  pay of the chief operator/superintendent  is
    approximately  the same  as the shift operators.
                                                  32

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    This  pay differential does not recognize the chief
    operator's additional responsibility.

•   It is very difficult to sample the sludge discharge
    lines  from the sedimentation basins.

•   Additional process control testing should be done
    to  provide more of a  basis  for process  control
    decisions. Examples of further testing  would
    include  more frequent analysis of  raw water
    turbidity  and alkalinity,  along  with measurements
    of  turbidities  of  the  water  leaving  each
    sedimentation basin and filter.
Projected Impact of a CCP
Results of the CPE  indicated that plant performance,
based  on daily  measurements of turbidity  from the
clean/veil and a filter turbidity profile conducted during
the evaluation,  was in compliance with applicable
drinking water regulations.  The plant monitoring data
also showed very consistent plant performance for the
12-month period evaluated. As a result, a CCP was
not recommended at Plant 3.
                                                  33

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  Plant 4

  Facility Description
  Plant 4 is owned and operated by the county water
  and sewer district.  It was  constructed in  1970  and
  serves  approximately  81 connections, including  the
  school. It  is a packaged,  conventional plant and its
  processes  include  pre-sedimentation,  flocculation,
  sedimentation, and filtration.

  A stream fed largely by return flows from the local
  irrigation district,  supplies the  plant.  Historically,  the
  creek flowed only  intermittently, but the importation of
  irrigation water with subsequent water losses to creek
  drainage have  significantly  increased stream  flows.
  These artificially increased stream flows, coupled with
  naturally  erosive  soils,  have  caused  a severe
  sedimentation and turbidity problem in  the creek.

  Plant flow  records indicate an  average  daily  water
 production  of 0.4 Us {10,000 gpd)  in the winter and
 2.6 Us  (60,000 gpd) in  the summer. Flow  records,
 obtained from the plant effluent meter, do  not include
 water used for filter backwash.

 The  CPE  did not determine  the  accuracy of  the
 effluent  flow meter, but the inconsistency  of readings
 taken over the  day  indicated a problem  exists. The
 influent  flow rate  is  measured by a rectangular weir
 located just prior to the flocculation basin.

 At the time of the site visit, the influent flow rate was
 3.8 Us (60 gpm).  The plant operates  at this rate for
 various hours per  day depending on demand. Plant 4
 (see  Figure 4-15)  includes  the  following unit
 processes:

 • Manually-operated, 2-hp centrifugal raw water pump

 • 22.7 million-L (6 mil gal) earthen pre-sedimentation
   basin

 • 1.5-hp, 3.8-L/s (60-gpm) turbine-type settled water
   pump

 • Chemical  addition  of alum  and  polymer  without
   flash mixing; both  alum and polymer are mixed  in
   batches in 189-L  and  114-L  (50-gal and 30-gal)
   tanks, respectively

 • 1.2-m x  1.2-m   (3.8-ft  x 4-ft),  2,290-L  (605-gal)
   flocculation chamber with a constant-speed, vertical
   paddle wheel

•  0.9-m  x  1.6-m  (3-ft x 5.4-ft),  2,290-L  (605-gal)
   sedimentation chamber with 6-degree tube settlers

•  0.9-m  x 1.2-m (3.1-ft x 4.1-ft) mixed media  filter
   with perforated pipe underdrain system
  • 1.5-hp,  3.8-L/s  (60-gpm)filtered  water pump (to
    clearwell)

  • 5-hp, 14-L/s (220-gpm) centrifugal backwash pump

  • Chlorination system  consisting  of  a  calcium
    hypochlorinator;  solutions  are  made as needed in
    189-L (50-gal) batches

  • 45,420-L (12,000-gal) clearwell

  • Two high-service centrifugal pumps: one 7.5-hp, 5-
    L/s  (80-gpm), and  one 3-hp,  capacity unknown,
    backup

  Raw water is pumped through a 10-cm (4-in) line from
  the creek to the pre- sedimentation basin. The 1.5-hp
  turbine  pump delivers water  from   the  pre-
  sedimentation basin through a 5-cm (2-in) line to the
  plant. This  pump is started  automatically by a float
  control in the  clearwell and the flow rate is regulated
  by  a float-controlled  valve  in  the  chemical  mix
 chamber.

 Alum and polymer are  added in line to the raw water
 prior to  the  chemical mix chamber.  The manufacturer
 originally designed this  basin for the addition of calcite
 to stabilize the raw  water. Some mixing, but no flash
 mixing,  is provided  both  in the line  and through  the
 chamber. After chemical addition, the water flows over
 a rectangular weir and  into a single-stage flocculation
 basin  with  a detention time  of 10  minutes  at both
 design  and  operating  flows.  The flocculator is a
 constant-speed (12 rpm), vertical paddle wheel type.

 Following flocculation, the water flows into the settling
 chamber equipped  with  6-degree  horizontal tube
 settlers. Settled water flows over a weir onto a mixed
 media  filter  equipped  with  a  perforated  pipe
 underdrain. The filter  operates  on  a  constant
 rate/variable  head basis;  a  float-controlled effluent
 valve regulates flow  rate. Design filtration rate  is 293
 m3/m2/d (5 gpm/sq ft); the  operating filtration rate was
 determined to be 281 m3/m2/d (4.8 gpm/sq ft). Water
 is pumped out of the filter to the clearwell.

 Backwash is initiated  manually or  automatically  by
 headloss  across the filter; the filter is  not equipped
 with a surface  wash. The backwash flow rate  of 13.9
 Us (220  gpm)  corresponds  to a wash rate  of 978
 m3/m2/d (16.7 gpm/sq ft). Filter backwash water flows
 by gravity  to  an earthen storage pond  located
 northwest of the plant, adjacent to the stream.  Sludge
from the tube settlers is removed  with the backwash
cycle.

Filtered  water  is  disinfected  with a  calcium
hypochlorite solution  within the clearwell and pumped
approximately 2.6 km (1.6  mi) to  the town reservoir
                                                  34

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Figure 4-15. Plant 4 process flow diagram.
                                                           35

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 Figure 4-16.  Plant 4 performance potential graph.
     Unit Process
                                           20
                     Flow, gpm
                  40          60
                                                                              80
                                                                                         100
     Raw-water Pumps


     Flash
     Flocculatlon1
      Detention time, min


     Sedimentation2
      SOR. gpm/sq ft


     Filtration
      HLR, gpm/sq ft


     Disinfection
      Contact time, min



     High-service Pumps
Not Rated


None
         21 i
      1.4
      1.7
                  3.3
      600
                 300
                             200
                                         150
   i 45-m!n HOT for sweep floe; 22.5-min HOT for direct filtration.
   2 Based on SOR = 2 gpm/sq ft
                                                               Operating and
                                                                Design Flow
(capacity of 50,000 gal [189,250 L) through a 10-cm
(4-in) line.

Major Unit Process Evaluation
The performance potential graph is shown in Figure 4-
16. The slashed vertical line on the graph represents
both the design and operating flow rate of 3.8 L/s (60
gpm).

As seen in Figure 4-16, the raw water pumps were not
rated because actual  pump output was not known.
The high-service pumps  were  rated  at  4.4 L/s (70
gprn), slightly above the design flow. The flocculation
basin was rated at 0.8 Us (13 gpm) when operated in
the sweep mode of coagulation and  at  1.6 L/s (26
gpm) when operated in the direct filtration mode. The
rated flow  was doubled  for direct  filtration because
shorter flocculation times  are acceptable in  this
operational mode. The flocculation  basin was derated
because it  is a single-stage unit and only provides  10
minutes of detention time at a 3.8 L/s (60 gpm) flow
rate.  Single-stage flocculation  and short  detention
times make  formation of  an  adequate  floe  more
difficult.
                  The sedimentation basin  was  rated  at  1.8  L/s (28
                  gpm) or 117 m.3/m2/d (2.0  gpm/sq ft) surface overflow
                  rate (SOR)  based on the capability of the tube settler
                  to produce  a clear water with the  existing  raw water
                  conditions.  The design surface overflow rate  of 251
                  m3/m2/d (4.28 gpm/sq  ft)  is  too high  given the raw
                  water  conditions and  has  resulted  in excessive
                  carryover of solids to the filter.

                  The mixed media filter was rated at the design flow of
                  3.8 L/s (60  gpm), which corresponds to a loading rate
                  of 293 m3/m2/d (5 gpm/sq  ft). The backwash rate was
                  also rated  at design,  for  up to 1,171 m.3/m.2/d (20
                  gpm/sq  ft).  The condition of  the media must be
                  restored (mudballs eliminated) and  the support gravel
                  and underdrain integrity must  be verified to justify this
                  rating. The backwash cycle  must  be extended  and
                  surface wash facilities  should be added or the  filter
                  will again become a major limiting factor at this plant.

                  Disinfection contact time was rated at 2.0 hr at flows
                  of up to 6.2  L/s (98 gpm).  This rating was justified
                  because of  the long transmission line to town and the
                  189,250-L (50,000-gal) storage reservoir.
                                                   36

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The  performance potential graph  indicates  that  the
plant  capacity  is  limited  by the  flocculation  and
sedimentation unit processes. To achieve acceptable
finished water quality, the  plant capacity may have to
be limited to about 1.9 Us (30 gpm) and  operated for
longer periods of time to produce the daily amount
required.

Performance Assessment
A review of the finished water quality monitoring  data
submitted to the State  indicate  that the  plant is
operating at the current MCL for turbidity,  1.0 NTU, on
a monthly average.  However, much of this data was
collected from the storage reservoir located in town,
2.6 km (1.6 mi) from the plant. Sampling  at this point
violates  the  regulations and   intent of the  law.
Unreported records  of  turbidity data taken  directly
from the filter reveal that numerous excursions above
the 1.0 NTU occurred on a regular basis for several
months.  These  data  indicate  the plant  will have
difficulty meeting the SWTR turbidity MCL of 0.5  NTU
for 95 percent of the time. Figures 4-17,  4-18 and 4-
20  depict turbidity  data from  plant  records,  while
Figurs 4-19 shows turbidity  data generated  from
special CPE studies.

Inspection of  the  filter revealed  a  heavy  layer of
chemical floe  on the  media surface  and  numerous
mudballs within the  anthracite.  The depths  of media
were  found to be adequate; however, probing of the
media indicated the support gravel varied by as much
as a  couple of inches in some areas of the filter. In
the past 18 years of operation, the filter media has
"solidified" to a concrete-like state twice,  the last time
about 5 years ago.

Media removal necessitated the use of a jackhammer.
Recently, the clearwell and  in-town  reservoir were
both  cleaned for the first time. Four 189-L (50-gal)
barrels of media and sediment were removed from the
clearwell and a considerable amount of sediment was
removed from the finished water storage reservoir in
town.

Inspection of the automatic backwash cycle indicated
that the  backwash time was  inadequate  to  clean the
filter  media. This, coupled with the lack  of a surface
wash, has allowed  the filter to  accumulate  mudballs.
The  inadequate backwash not  only  results in costly
replacement of the  media, but also makes production
of an acceptable finished water quality impossible.

Performance-Limiting Factors
The  factors  identified as having  a  major  effect on
performance  on a  long-term   repetitive  basis are
summarized below in order of priority:

 1.  Water Treatment Understanding - Operation: The
    operator is newly hired and, while enthusiastic and
    willing to learn,  has had no  training or background
    in the science of water treatment.
2.   Process Control Testing  -  Operation: Testing  to
    monitor the effectiveness of the treatment process
    is  inadequate.  The  available  data  clearly
    substantiates  turbidity  MCL violations.  (See
    Figures 4-17 through 4-20.) During certain times,
    unacceptable  water  is supplied  to  the public,
    exposing  users  to  an  unacceptable  risk  of
    contracting waterborne diseases.  At  a minimum,
    turbidities  should be  monitored in the  plant
    influent, sedimentation basin  effluent,  and filter
    effluent several  times each day. Jar testing should
    be  done  daily  or  at least when  raw water
    conditions change, to fine-tune chemical dosages.
    Continuous-recording, in-line  turbidimeters would
    be  very  beneficial in  providing   information  for
    optimizing process control.

3.   Plant  Coverage - Administration: The  operator
    makes one brief visit to the plant each day, which
    is not adequate to perform proper process control
    testing,  experimentation,  and  adjustments.
    Addition of continuous-recording turbidimeters and
    appropriate alarms could reduce the time spent at
    the plant, but a minimum of 2  hr each day will still
    be required for process control testing.

4.   Flocculation -  Design: The  plant  design  only
    allows for single-stage  flocculation  and  the
    detention time is too short to allow optimum floe
    formation before water flows to the sedimentation
    chamber.  The  effect of  flocculation  may be
    reduced  if the  plant could be run  in  the  direct
    filtration mode.  However, the  plant flow rate may
    need  to  be reduced to overcome  flocculation
    deficiency.

Factors identified as having either a minimal effect on
a routine  basis or a major effect on  a periodic basis
were prioritized and are summarized below.

1.  Laboratory Space and Equipment -  Design: The
    operator  has   no  equipment  other  than  a
    turbidimeter to  perform  the  necessary tests  to
    determine  raw  and  finished  water  quality. The
    accuracy  of the  meter cannot even  be verified,
    because  of a lack of equipment.  There is no jar
    testing  or other equipment and supplies  for
    process control testing.

2.  Operator Pay - Administration: The operator pay is
    too low  to compensate  the operator for  the
    number of hours necessary to run the plant
    properly. This  pay does not offer an  incentive for
    keeping  qualified operational personnel  or for
    providing adequate plant coverage.

3.  Alarm Systems - Design: Because of a lack of an
    alarm system,  particularly  on the finished water
    turbidity,  unacceptable water has been pumped
    into the  distribution  system on many  occasions.
    Without  alarm  systems  and  with minimal plant
                                                   37

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 Figure 4-17.  Plant 4 turbidity profile.
    Turbidity, NTU

       3.0
       2.5
       2.0
       1.5
       1.0
 A
Unreported
 Maximum

 A
                                                                                           ^*
1 ' '
/ ' '
. \ 1
	 t-r 	
V
Regulatory Maximum
^--*^
= 1.0 NTU
— v 	
\
                                                                  Desired Operating = 0.1 NTU
                 6/87
8/87
                                              10/87
                                                              12/8

                                                              Date
                                              2/88
                                                            4/88
                                                                           6/88
Figure 4-18.  Plant 4 turbidity profile, August 1987.

  Turbidity, NTU

   3.0

                Reported
  2.0
  1.0
                            Regulatory Maximum = 1.0 NTU
                                 Figure 4-19.  Plant 4 turbidity profile before and immediately
                                              following backwash.

                                  Turbidity, NTU
                                     1.0 i-
                                                                    0.8
                                                                    0.6
                                                                    0.4
                                                                    0.2
         	(DesiredOperating 0.1 NTU
             """""   j   |   i   f  |   i
        17      20          24

                      Day of Month
          28       31
                                                       Immediately Following Backwash
                                                  Prior to Backwash

                                                    I	I
                                                                                                           I
                                                    10           20         30

                                                      Minutes After Backwash
                                                                         40
                                                            38

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Figure 4-20.  Plant 4 turbidity profile , January, 1988.

  Turbidity, NTU          20 +            20 +
                                                            20 +
                          20 +
    20
    15
    10
            Unreported
             Maximum
                  Reported
                     I
                               Regulatory Maximum = 1.0 NTU

                                           	I
 I
                                 10
15           20

  Day of Month
                                                                       25
30
    coverage, the operator is not aware of the water
    quality being supplied to the town.

4.  Staff Number -  Administration: The  district needs
    to  have a  backup  operator, so that the  plant
    manager can leave town for business or personal
    reasons without leaving the plant unmanned.

5.  Flash Mix -  Design: Lack of a  flash mix unit will
    limit coagulation effectiveness  and increase the
    chemical  requirement,  particularly  if the plant  is
    run in the direct filtration mode.

6.  Sedimentation - Design: The surface loading rate
    within the  sedimentation chamber  is too  high to
    allow floe to settle  prior  to flowing  to the filter.
    Better  settling  would  improve  or  lengthen filter
    runs. Operation  in the direct filtration mode would
    eliminate the sedimentation  basin  as a potential
    problem since  the  floe  that   is  produced  is
    filterable, but not settleable.

In addition to   the  above major  factors  limiting
performance,  other factors identified  as having  a
minor effect were noted during  the  evaluation.  Action
taken to address these factors may  not noticeably
improve  plant performance,  but may  improve the
efficiency of plant operation:
        • Lack  of a preventive maintenance program  may
          result  in  excessive  equipment downtime, which
          could  be significant  since  there  are no  backup
          systems.

        • Lack of filter surface wash  may be contributing to
          the inefficient washing of the filter.

        • Lack  of standby units for  key equipment could
          cause  periods of plant downtime.

        Projected Impact of a CCP
        Results of the CPE indicated performance was limited
        by a number of factors in operation, administration,
        and design. The evaluation team judged that a CCP
        could help the plant make significant  improvements in
        finished water quality. However, design limitations may
        require the  plant to operate  at  a reduced  rate  to
        produce  an acceptable finished water quality.  In
        addition,  since many of the limiting factors  are in the
        areas of administration and design, some minor capital
        improvements  must  be  made   and   greater
        administrative  support to the  plant  (i.e.,  higher
        operator  salary) must  be  provided   to  significantly
        improve plant performance.
                                                   39

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  Plant 5

  Facility Description
  Plant 5 is a direct filtration plant that was installed in
  1978 to replace an older pressure filter. At the time of
  the CPE, the system had a total of 1,122 connections.
  Water for the plant is supplied from the southeast end
  of a multiple use  lake located about 29 km (18 mi) to
  the northwest.

  The  plant's  water  treatment processes  include
  coagulant  chemical  feed  (alum  and polymer),
 flocculation  in  a  reaction  basin,   optional  pre-
 chlorination  and  non-  ionic  polymer filter aid feed,
 filtration  through four  dual  media filters,  post-
 chlorination, and gravity flow from the plant to storage
 and  distribution. The  plant was designed for a flow
 rate  of 131 L/s (3 mgd). Plant flow records for a 12-
 month period indicated  an average daily flow of 26 Us
 (0.6  mgd).  Average  monthly flows during  the  same
 period were 12-50 L/s  (0.28  and 1.16 mgd). Plant 5
 (see  Figure  4-21)  includes  the  following  unit
 processes:

 • Two 100-hp, 125-L/s (1,980-gpm), vertical turbine
   raw water pumps

 • 36-cm  (14-in) propeller influent  flow meter at  the
   plant

 • Chemical  addition  of alum and  cationic  polymer
   without flash mixing

 • Three-compartment  "reaction" basin  that allows
   mixing  and detention time for flocculation, 6.1  m
   (20 ft) in diameter, with a water depth of 2.3 m (7.6
   ft)

 • Four dual media filters, each 3.5  m  (11.5 ft) square
   and 2.4 m (7.75  ft)  deep,  with  heater/lateral-type
   underdrains

 • Two 60-hp, 167-L/s (2,650-gpm)  vertical  turbine
   backwash pumps

 • 10-hp,  7-L/s  (112-gpm)  vertical  turbine  surface
   wash pump

 • Two 378,500-L  (100,000-gal)  hypalon-lined
   backwash water storage basins

 • Two submersible backwash water recycle pumps

 • Gas chlorination system

 • Two 3.8  million-L  (1  mil-gal), steel ground  level
   reservoirs

Water is pumped to the  plant through a pair of 30-cm
 (12-in) transmission mains.  One pump is used  at a
time and the pumps automatically alternate each time
 one of them  stops.  The pumping rate through the
 plant was measured at approximately 136  L/s  (3.1
 mgd),  at  the  time of the visit. This is the "normal"
 plant flow rate and remains constant.

 The influent flow meter was found to measure almost
 13  percent less flow  than was  calculated to  be
 entering the clearwell. Meters typically measure less
 flow with  age,  so  the  meter  may  need  to  be
 recalibrated.

 A valve controls the flow to the plant during startup of
 the  raw  water pumps. An  orifice plate  is  located
 downstream of  the  valve  to  regulate  pressure for
 optimum operation.

 Alum and  a cationic  coagulant  polymer are added to
 the influent after the orifice  plate. Typical feed rates
 were 5-10 mg/L for alum and 0.1 jng/L for the cationic
 polymer.   No  flash  mixing  is  provided;  however,
 moving the chemical  feed points to the orifice plate
 would probably result in a hydraulic flash mix. At low
 alum feed rates  in a direct filtration plant,  some  type
 of flash mixer must be provided.

 The  three compartment reaction  basin allows some
 flocculation to occur before filtration. Flow of the water
 through the baffled compartments provides hydraulic
 "agitation" of the water to promote floe formation. No
 outside energy is input to  the water.  The reaction
 basis has apparently been designed  to  decrease
 turbulence  as  flow   proceeds  through  the
 compartments. Approximately 8 minutes of detention
 time  are provided in the reaction basin at the normal
 flow rate.

 Chlorine and a non-ionic polymer can  be added just
 ahead of  the filters,  but chlorine normally is  added
 only after filtration. The non-ionic polymer, Serapan, is
 added ahead of the filters during some  periods of the
 year, for example, in winter when turbidities are low.

 Water then enters an open influent channel where it is
 distributed  to the dual media filters.  Flow through the
 filters is regulated by  effluent valves. As the headloss
 across the filter builds up, the effluent valve gradually
 opens to. counteract this increase.  Since the influent
 flow to each filter cannot be equally split, the flow rate
 through each filter is unknown. 61 cm (24 in) of 0.90-
 mm effective size anthracite and 15 cm  (6 in) of 0.45-
 to 0.55-mm effective size silica sand lie above the 53
 cm (21  in)  of layered  support gravel. A header/lateral
 piping underdrain system is located at the bottoms of
 the aluminum filter boxes. The filtration rate  under
 normal plant flow conditions is 234  m3/m2/d (4 gpm/sq
ft).

One interesting feature of the filters is the design of
the discharge header. The  header profile rises  in
elevation just before the  water is discharged into the
clearwell. This  discharge pipe then terminates just
                                                  40

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Figure 4-21.  Plant s process flow diagram.
                 a|
                 5 flS
                 a cซ
                 (3 2
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                                             41

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  above the floor of the clearwell,  creating a negative
  head in the discharge header from the filters. The
  intensity of the negative head depends on the amount
  of headless across the filters, the plant flow rate, and
  the  depth of water in the  clearwell. A plug  can be
  removed from the  top  of the  tee  fitting,  thus
  eliminating the  negative  head condition.  It is not
  known what effect this negative head condition has on
  the filter operation, but its  effects should be evaluated.

  Backwash is initiated by adjustable headloss controls.
  The two  60-hp  pumps each  provide 167 L/s (2,650
  gprn) of backwash  water  from the clearwell at 21 m
  (70 ft) of head. A rotating arm surface wash  system
  helps break up sediment  at the surface of the filters
  during backwash. The 10-hp surface washwater pump
  can provide 7 L/s (112 gpm) at 79 m (260 ft) of head.

  The  spent plant backwash water  is stored in the two
  hypalon-lined basins  adjacent to  the  plant.  After
  settling  overnight, the decant water is recycled  back
  into the plant by two submersible pumps. The valve
  described previously holds the flow rate through the
 plant constant during recycle of the backwash water.

 The production of the backwash pumps was restricted
 by a butterfly valve to  about 118 L/s (1,870 gpm)  each
 to prevent excessive media loss and disruption during
 backwash. This  represents a  backwash  rate of only
 about 820 m3/m2/d  (14 gpm/sq  ft); the backwash
 pumps are capable  of pumping as  much as  167 L/s
 (2,650 gpm),  or 1,171 m3/m2/d (20  gpm/sq ft).  Dual
 media filters  are typically  backwashed  at 878-1 171
 m3/m2/d (15-20 gpm/sq ft).

 Major Unit Process Evaluation
 The performance potential graph is shown in Figure 4-
 22. The raw  water  pumps appear to be capable of
 pumping  at the plant  design  capacity of  131  L/s (3
 mgd). During  the plant evaluation, the plant flow rate
 was measured  by drawing down  the  clearwell  and
 measuring the average rate at which it filled with time.
 This rate was  measured at  136 L/s (3.1 mgd)).

 The reaction  basin  was not a typical  design  and,
 therefore,  was rated  in  terms  of  detention  time
 provided. A detention time  in flocculation  basins of at
 least  20  minutes normally  is desirable to  permit
 adequate floe  formation in cold water conditions. (The
 reaction  rates  of  the  coagulants  are  slowed
 considerably in cold water.) To provide a 20-minute
 detention  time, the plant flow rate  would have to be
 decreased to  57 L/s (1.3 mgd). Achievement of this
 rate would require  the raw  water pumps  to be
 restricted in their output during the winter months.

 During warm  water  conditions,  the  flow  rate
theoretically can be increased because reaction rates
of the coagulant chemicals are higher.  The  typical
minimum  flocculation time for  warm water,  which
appears in the design standards,  is  10  minutes. To
  provide 10 minutes, the plant flow rate would have to
  be reduced to 114  L/s (2.6 mgd). Further evaluation
  would be required to  determine the  actual detention
  times necessary for  successful flocculation.

  The filters are the weakest major process. The most
  significant factor  affecting  filter performance is air
  binding.  Air binding (accumulations of air within  the
  filters) has  been  a problem  since  the  plant  was
  constructed. It is believed that the air coming  into the
  plant from the lake is very high in dissolved gases. As
  water flows into the  plant from the transmission pipe,
  the  pressure  on the water is relieved,  allowing  the
  dissolved gases to escape. The air accumulations  are
  so serious that the filters have to be allowed to "rest"
  for several minutes prior to backwashing to allow  the
  gases to  escape, so  that  they  will  not  disrupt  the
  support gravel and  filter  media  during  backwash.
  Based upon  the uneven surface of  the  top of  the
  media in one  filter,  it  is possible  that accumulations
  have disrupted  the  support  gravel  in the  past. If
  disruption of the support gravel has occurred, it would
  need to be  removed from the filter(s) and replaced.
  Further investigation  is  needed to  evaluate this
  potential problem before taking such drastic action.

  During air binding, the  effective  filtration rate through
 the filters  is increased  because the water  must flow
 around the air bubbles. The net area of the filters is
 therefore reduced,  resulting in  an increase  in effective
 filtration rate. The only way to reduce the filtration rate
 is to  either eliminate the air  binding  problem, or to
 reduce the plant flow rate. The plant is now operating
 at, or slightly above, the design filtration rate  of 234
 m3/m2/d (4 gpm/sq ft) or 136 L/s (3.09 mgd). Because
 about 20  percent of the finished water must be used
 for backwash  water, the effective filtration  rate  is
 reduced to 187 m3/m2/d (3.2  gpm/sq ft) or 107  L/s
 (2.44 mgd). After observing the amount of air released
 from  the filters, the evaluation team estimated that  the
 effective filtration rate of the filters may  have to  be
 reduced to about 117 m3/m2/d  (2 gpm/sq ft) or 67  L/s
 (1.52 mgd).

 The  automatic filter backwash  cycles  (headloss
 initiated) did not appear to be long enough to properly
 clean  the  filters. The  water was  still dirty  as the
 backwash cycle ended.  Improper cleaning of the filters
 can lead to poor treatment and  short filter runs.

 Performance Assessment
 Finished water quality data  from the  past  year
 indicated that the plant  was operating  within the 1.0-
 NTU  standard  for  finished  water turbidity, although
 incoming turbidities are extremely  variable.  Winter
 turbidities are often  less than 5 NTU, and usually less
 than 10 NTU, while spring and summer turbidities can
 vary widely,  even  within a  given day.  Prevailing
westerly winds  often stir up sediment in the relatively
shallow lake, resulting in raw water turbidities of 50-
280 NTU.  Monthly average turbidities are reported
                                                  42

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Figure 4-22.  Plant 5 performance potential graph.


    Unit Process
                Flow, mpd
    Raw-water Pumps


    Reaction Tank
      HOT, min



    Filters^
      HLR, gpm/sq ft


    Chlorination
      Cobntact time, min
    Winter - 20 min
      (1.3 mgd)
Summer - 10 min
   (2.6 mgd)
  26
                          13
          (1.5 mgd)
 (2.4 mgd)
360
                        180
                                                12'
                                                                                         Design
                                                                                        Capacity
    Flow reduced to 2.44 mgd to account for 20 percent of the production being used for backwash water.
    The flow may have to be reduced even further (to approximately 1.5 mgd) because of air binding.
 typically at 0.5 NTU  or less, but turbidities of 0.5-0.6
 NTU range were reported for a few months.

 Finished  water  quality data is taken from  the plant
 potable water system, which  pumps water from  the
 clearwell. Readings are typically taken at about 9 a.m.
 after the  plant has been  shut down overnight. Figure
 4-23 shows, under current operating conditions,  the
 number of days  each month that Plant  5 would be in
 violation  of the SWTR  effluent turbidity  standard,
 which will require that finished water turbidity be  0.5
 NTU or less at least 95 percent of the time.

 Inspection  of Filter 2 after dewatering  did not detect
 the presence of any mudballs; there was, however,
 deep penetration of the floe into the anthracite. This in
 itself is not necessarily indicative of a problem, but a
 variation  of about 5  cm (2  in)  in the elevation of the
 top  of the anthracite media indicates a potentially
 serious problem with the  condition of  the  support
 gravel.

 The presence  of filter sand  and  anthracite in  the
 clearwell  also  indicates  a potential  problem.  This
 material  was cleaned out of the clearwell  previously
 but has since accumulated. If the support gravel were
 in proper  condition,  the filter  sand and  anthracite
 layers would not  break through to  the underdrains.
 Readings taken after backwash of Filter 2  during the
 site visit indicated  that  the filter effluent  turbidity
 exceeded  1.0 NTU.  This  is of concern both for the
 present  standard of  1.0 NTU  and the  proposed  0.5-
 NTU standard.  These data are presented in a graph in
 Figure 4-24.
               Over the past several years, the State has completed
               microscopic  particulate examinations  (MPEs) of the
               finished water to determine the effectiveness of the
               filtration process. These have shown that the finished
               water  contains  a large amount  of  particles  (algae,
               insect  eggs,  etc.), which  indicates that, at times, the
               filters are not operating  well.

               Performance-Limiting  Factors
               The factors  identified  as having a  major  effect on
               performance on  a long-term repetitive  basis are
               summarized  below in order  of priority:

               1.  Operator Application  of  Concepts  -  Operation:
                   Varying  raw water quality requires changes  in
                   chemical feed  rates  and plant flow rates  to
                   maintain  acceptable  finished water quality.  The
                   plant had no organized  process control program to
                   provide information to base operational decisions
                   upon.  Although  the  operators   had  a  good
                   understanding of water treatment, they were not
                   applying  that knowledge fully.

               2.  Process  Control  Testing - Operation:  Proper
                   operation of a direct filtration plant requires regular
                   process  control testing so that  chemical doses
                   can be optimized. Jar teb^ig, followed by filtration
                   through  Whatman  #40  paper  filters,  is  a
                   reasonable  simulation of the  direct  filtration
                   process. This regular testing was not  being done
                   at the  plant.

                3.  Filtration - Design: Turbidity measurements taken
                   .at the time of the  evaluation and MPE testing
                                                     43

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  Figure 4-23.  Plant 5 potential for SWTR compliance.
              Aug   Sep   Oct  Nov  Dec   Jan   Feb  Mar  Apr   May   Jun   Jul
                                                                                        Days Allowed
                                                                                        Above 0.5 NTU
    done by the State demonstrate that the filters do
    have a performance  problem. The presence  of
    filter media in the clean/veil  indicates that the
    support gravel may have been damaged  in the
    past. If the support gravel  is in  fact damaged,
    replacement to the media will be necessary. Filter
    capacity  and  finished  water quality  is  being
    affected by severe air  binding. Periods of high
    turbidity also require frequent backwashing, which
    further  reduces  plant  capacity.  If the  support
    gravel is in good condition,  then the filters could
    be rated as a lower priority factor and the filtration
    rate decreased because of the air binding problem
    and backwash  water requirements.

Factors identified as having either  a minimal effect on
a routine basis, or a major effect on a  periodic basis
were prioritized and are summarized below.

1.  Turbidity - Design: The turbidity of the raw water
    often exceeds  that normally recommended for the
    direct filtration  treatment mode. During periods of
    high turbidity, it may be necessary to reduce plant
    flow  rates  to  produce  an  acceptable finished
    water. Nearly constant backwashing  may also be
    necessary because of the solids load to the filter,
    which will reduce the effective plant capacity.

2.  Plant Coverage -  Administration: The plant is not
    attended on  weekends  and the  operators are
    often  away from the  plant  during weekdays
    performing  other  duties. As a  result, periods of
    poor finished water quality could go undetected.

3.  Lack of Standby  Units - Design: There  are  no
    standby alum and polymer feed units. Failure of
    one of  the units would severely  affect  plant
    performance.

4.  Automated Process Monitoring - Design: A lack of
    continuous  monitoring  turbidimeters  on the  raw
    water quality at the lake pumping station and  on
    the  effluent line  from  each filter  makes  plant
    operation more difficult.  Turbidity monitoring  on
    the raw  water would allow increases  in raw water
    turbidity to be anticipated, so that treatment could
  -  likely be improved. Monitoring of the  filter effluent
    quality  would provide  information necessary  to
                                                   44

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Figure 4-24. Finished water turbidity profile after backwash of filter 2 - Plant 5.
                                       Backwash
                                       Recycle
                                       Pump On
                                                         Minutes
    adjust chemical  feed  rates  and,  therefore,
    optimize filter performance.

5.  Reactor Basin - Design: The reactor basin may
    provide inadequate  detention  time  to  allow
    chemicals  to react and flocculate  during  cold
    water conditions. As a result, the plant  flow may
    have to be reduced substantially during the winter.

6.  Inoperability  Due  to  Weather  -  Design: As
    discovered  during the summer  of 1985, drought
    can severely  impact the availability of water from
    the lake. The raw  water intake  is located  in  a
    shallow corner  of  the  lake and  considerable
    attention has  been given to relocating the intake
    to  a deeper portion of the lake.  An engineering
    study has  been completed that evaluates the
    alternatives for another intake location.

In addition  to the  above  major  factors  limiting
performance, other minor factors were noted during
the evaluation. Action taken to  address these factors
may not noticeably  improve plant  performance, but
may improve the efficiency of plant operation:

•  Funding the  operation  of  the  wastewater system
   through  water  revenues  is  not  a good  practice.
   Each utility should be self sufficient.
•  Better communication of priorities to the plant staff
   and better teamwork among  staff members could
   improve plant performance.

•  Return of spent backwash water to the influent can
   result  in increased  raw water turbidities  and  a
   change in raw water chemical  characteristics.

•  The alum and cationic polymer feed points provide
   no flash mix of the chemicals.  Movement of the
   chemical feed points to just prior to the orifice plate
   would  provide better mixing.

Projected Impact of a CCP
It  was projected that  a CCP  would  help Plant  5
achieve  better performance.  Results  of the  CPE
indicated that  the plant was limited by a number of
factors, primarily in operation and design. Because of
the design limitations, the plant would need to  reduce
its operating rate to produce an acceptable finished
water  quality.   Some   capital  investment  could be
necessary, depending upon the condition of the filters.

It was recommended that the city continue its efforts
to  construct a  new water intake on the  lake.  The new
intake would appear to improve the  quality of the raw
water, as well as the reliability of the water source.
                                                  45

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  CCP Results
  A CCP was initiated, at which time the plant flow rate
  was reduced so that design-related  limitations could
  be addressed.  During the initial  site visit, the CCP
  team developed a daily data sheet and implemented a
  procedure  describing  process  control  testing.  In
  addition,  procedures were developed  for calibrating
  chemical feeders and calculating chemical dosages  so
  that chemical feed rates could be accurately applied.
  Special studies were  implemented to determine the
  effect of operating the plant at a reduced flow rate and
  operating the filters without a negative pressure.

  At  the  conclusion  of the  first visit, the  plant was
  operated at 69 Us (1,100 gpm) rather than at 132 L/s
  (2,100 gpm)  and a plug  was  removed from the filter
  effluent header to release the negative pressure from
  the filter. Chemical  feed rates were not changed. The
  CCP team developed an action list and assigned tasks
 to the  operating staff and administrators with due
 dates to ensure activity continued until the next site
 visit.

 During an additional two site visits and weekly  phone
 consultation sessions,  the CCP team explained the
 conduct and  interpretation of  the  jar test/filter  paper
 procedure to the operating staff.  This, coupled with
 activities  from  the first  site visit,  launched  full
 implementation  of  the process  control  program,
 including evaluating  raw water quality and making  a
 determination of the correct coagulant  and filter aid
 feed rates.

 The  only physical  change  to the  plant was the
 relocation  of  the feed points  for  alum and  cationic
 polymer addition to take advantage  of a hydraulic flash
 mix at an orifice  plate located  in the influent piping.
 City administrators were also convinced to allow time
 for the operating staff to  remain at the plant so that
 they could conduct process control testing and  make
 plant adjustments.

 Figure 4-25  shows the significant improvement in
 plant performance achieved by Plant 5 during the
 conduct  of the  CCP. Plant  operation  improved after
 reducing  the plant  flow  rate  and  eliminating the
 negative pressure on the  filter  bottoms in  April, but
 performance remained  erratic  until process control,
 including chemical adjustments, was implemented in
 July. After July, plant finished  water turbidities
 remained very consistent  at about 0.1  to  0.2  NTU
 through the duration of the project, even though raw
 water turbidities  varied widely  (Figure 4-26).  Plant
 finished water quality remained below  0.3 NTU  even
 when the  raw water  turbidities reached  70  NTU,
 because  the operating staff consistently monitored
 varying raw water quality and responded by changing
chemical feed rates.

 Plant performance  was especially  impressive  since
influent turbidities frequently exceeded values thought
 to be treatable with direct filtration (e.g., less than 50
 NTU). Another  indication of  improved  performance
 was that  filter effluent turbidity following a  backwash
 did not exceed  0.3 NTU and  returned to 0.15 NTU
 within minutes after the wash.

 The CCP  proved  that  the   plant  could  achieve
 compliance with SWTR turbidity requirements without
 major capital improvements. City administrators had
 planned  on spending an  estimated  $1,000,000  on
 construction of sedimentation basin facilities  and
 related improvements. After the CCP, they decided to
 delay any  construction until water demands required
 the plant  to be operated at higher  rates.  The plant
 staff developed  increased confidence that  excellent
 quality water could be  produced despite  high  raw
 water turbidities, and they developed a level of pride
 that did not allow them  to accept marginal finished
 water quality.  In addition,  the jar  test/filter  paper
 procedure  proved  to be  a  valuable  process control
tool that  allowed  accurate selection of  coagulant
doses.
                                                  46

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Figure 4-25.  Finished water turbidities during CCP for Plant 5.
                      -89  12-Moy-89  21-Jun-89  31-Jul-89  09-Sep-89 19-Oct-89  28-Nov-89
Figure 4-26.  Raw water turbidities during CCP for Plant 5.
              80
70 -


60 -

50 -


40 -


30 -

20 -

10 -
                              T
                            no
               0 -
               02-Apr     12-May    21-Jun     31-Jul     09-Sep     19-Oct     28-Nov
                                                    47

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 Plant 6

 Facility Description
 Plant  6 was built in 1916,  and  underwent major
 modifications in  1923 and  1960. To  date the plant
 serves approximately 5,000  people, with no significant
 industrial users.  The plant's  water  source  is the
 nearby river. The  plant  is a  175-L/s (4-mgd)  lime
 softening facility with pre-sedimentation, rapid mix and
 flpcculation (in a solids contact unit), filtration,  and
 disinfection. The  maximum quantity of water produced
 over a 12-month  period was 1,182 L/s (4.15 mgd) and
 the lowest was  17  L/s  (0.39  mgd).  Plant  flow  is
 measured  by a raw water meter ahead of the solids
 contact  unit,  and by a  master 'meter following the
 high-service pumps.

 The city is  currently  under a  compliance schedule
 from  the State to curtail  the  discharge  of untreated
 sludge into the river. The city has applied for funds for
 the construction  of sludge  handling facilities  and for
 other  plant modifications. Plant 6  consists  of the
 following unit processes (see Figure 4- 27):

 •  Four split-case centrifugal raw water  pumps: two 69
   L/s (1,800 gpm) and two 50 L/s (800 gpm)

 •  Pre-sedimentation basin divided into five sections,
   total volume of about 3.8 million L (1  mil gal)

 •  Three non-clog centrifugal  pumps (one  63-L/s
   [1,000-gpm]  and  two  94-L/s [1,500-gpm])  as
   intermediate pumps for transferring water from the
   pre-sedimentation basin to the solids contact unit

 •  Chemical addition of liquid cationic coagulant, alum,
   filter aid, pplyphosphate,  lime, soda water,  carbon
   dioxide, activated carbpn,  and gaseous chlorine

 •  Solids contact  unit with a total surface area of 144
   nr>2  (1,555  sq  ft)  and  a 3.1-m (10-ft) depth.  A
   mechanical 10-hp rapid mix unit is  located  in the
   solids contact unit.

 •  Recarbonation  chamber  to reduce  pH after
   softening

•  Seven single media sand  filters with  a total surface
   area  of  167 m2 (1,800 sq ft): three  in the plant
   addition  with surface area  of 33 m2 (360  sq ft)
   each, and four  in the old plant with surface  area of
   17m2(l80sqft)

-  Two chlorinators

•  487,130-L (128,700-gal) clearwell

•  Four vertical turbine high-service pumps: three 88-
   L/s (1,400 gpm) and one 63-L/s (1,000 gpm)
 Raw water is pumped  from the  river  to the  pre-
 sedimentation basin. Two of the raw water pumps are
 located in the basement of the  plant and  two are
 located in a  pumping station  north  of the  plant.  A
 hand-cleaned  basket  strainer  provides  preliminary
 screening for the two raw water pumps located in the
 plant basement.  The five separate chambers  in the
 pre-sedimentation basin are normally run in series, but
 may  be run in  series, parallel, or any  combination.
 Sludge is removed from the basin manually, and when
 the pre-sedimentation  basin is  cleaned the sludge  is
 discharged directly  to  the river. From  the  pre-
 sedimentation basin,  water  is  pumped by the three
 intermediate pumps to the solids contact unit. Chlorine
 may  be added  ahead of the  solids contact unit,  if
 necessary.

 In the solids contact  unit, alum, polymer,  lime, soda
 water, and activated carbon are added for softening,
 turbidity  removal,  and  taste and  odor  control.
 Flocculation and  rapid mixing both take  place  in the
 contact unit. From the solids  contact unit, water flows
 by  gravity  to  the recarbonation  chamber, where
 carbon  dioxide generated onsite  by burning natural
 gas  is  added   to  reduce  pH   after  softening.
 Polyphosphates are added prior to filtration.

 The design filtration rate is 117  m3/m2/d (2 gpm/sq ft).
 Filtration rates are controlled by an effluent regulator
 on  the  basis  of  flow  and headloss. The filters  are
 backwashed  with  finished  water from the clearwell
 pumped by one 189-L/s (3,000-gpm) backwash pump.
 Backwash water flow  is measured  by a Venturi  meter
 and totalized at the main instrument control panel.

 Filtered water  is disinfected  with chlorine  dosed at  a
 feed rate of 1-2  ppm. Disinfected water then flows to
 the clearwell.  The clearwell  detention  time  is 46
 minutes at a plant flow of 175 L/s (4 mgd).

 The three high-service pumps deliver the  water  to the
 distribution system.

 There are  no facilities available for the  disposal of
 sludge.  'Sludge  generated from cleaning  the  pre-
 sedimentation  basins,  solids contact  unit,  and  the
 spent filter backwash  water is piped untreated to the
 river.

 Major Unit Process Evaluation
 The performance potential graph is  shown in Figure 4-
28.  The raw water pumps were  rated at 208 L/s (4.75
 mgd),  based on  information  from  a  previous
engineering study. The pre-sedimentation basin was
rated  at 175 L/s (4 mgd) assuming that  a coagulant
aid  could be added prior to  the basin. At 175 L/s (4
mgd), the basin has a detention  time greater than the
3-hr  minimum recommended  by the  Ten  State
Standards.
                                                  48

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Figure 4-27.  Plant 6 process flow diagram.

-------
Figure 4-28.  Plant 6 performance potential graph.


    Unit Process
                      Flow, mqd
       12345
     Raw-water Pumps1


     Pre-sodlmontatlon Ponds2
      HOT, min



     Intermediate Pumps2

     Contact Units
      SOR. gpd/sq ft


     Filtration4
      Loading, gpm/sq ft


     Disinfection5
      Contact time, min



     High-service Pumps


     Sludge Handling
      643
                 1,286
Inadequate
                                                                           Rated Design
                                                                             Capacity
   i Based on previous master plan study.
   2 Based on addition of coagulant aids - detention greater than 3 hr minimum in Ten State Standards.
   3 Based on 1,440 gpd/sq ft.
   4 Based on 2 gpm/sq ft and assumes filter aid with labor-intensive backwash.
   s Based on 120-min contact time and total clearwell volume.
The intermediate  pumps were rated  at  167 Us (3.8
mgd),  slightly less than  the  175-L/s  (4-mgd)  design
capacity,  based  on  a previous  study.  Based on  a
surface overflow rate of 58 m3/m2/d (1 gpm/sq  ft), the
solids contact unit was rated at 96 L/s (2.2 mgd), well
below the plant design capacity.

The filters were rated at 228 Us (5.2 mgd) based on a
filtration rate of 117 m3/m2/d (2 gpm/sq ft). This rating
assumes successful use of a filter aid  and hand-raking
of the filters during backwash.

Because the clearwell has such a small volume in
relation to  total  plant production,  the  disinfection
contact time  was  rated  at only  8.8  L/s (0.2  mgd).
Current design  standards  require a  minimum
disinfection  contact time  of 2 hr,  but the  clearwell
provides only 46 minutes at 175 L/s  (4  mgd).  When
the plant produces water with  a turbidity greater than
                   1.0 NTU, the chlorine contact time must be adequate
                   to ensure disinfection  of  any pathogenic organisms
                   that  may have  passed  through  the plant's  previous
                   treatment steps.

                   The  high-service  pumps  are  rated  at 241  L/s (5.5
                   mgd).ln summary, the solids contact unit limits plant
                   capacity to 96 L/s (2.2  mgd)  during  periods of high
                   turbidity. An operational  rate greater than 96 L/s (2.2
                   mgd) may result  in increased solids carryover from
                   the solids contact  unit to the filters, with a subsequent
                   decrease  in filter performance and  overall  plant
                   performance. Also, if  bypass of the solids contact unit
                   becomes necessary,  provisions must be made to add
                   coagulants prior to filtration.

                   Performance Assessment
                   Finished water quality monitoring data  indicated that
                   the plant had been operating in  compliance with  the
                                                    50

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 current turbidity MCL  of less than  1.0  NTU on a
 monthly  average.  However,  the  MCL  had been
 exceeded on days within certain months. The highest
 finished water turbidities were noted  at a time when
 the  solids  contact  unit  was being  bypassed  for
 cleaning.  Plant records  indicated  that  no coagulant
 aids were added at times when the solids contact unit
 was bypassed, an unacceptable practice.

 Figures  4-29 through  4-31  show   selected plant
 operating  data.  The data shown  in  these  figures
 suggest  that the plant will experience difficulty  in
 complying with  the SWTR, which establishes a MCL
 for turbidity of 0.5 NTU  for 95 percent of the time.

 Performance-Limiting  Factors
 The factors identified  as having a  major effect  on
 performance on  a  long-term repetitive basis  are
 summarized below and  listed in order of priority.

 1-  Operator Applications of Concepts and Testing to
    Process Contro! - Operation: The operators had a
    good  understanding of water treatment but were
    not applying that knowledge fully.  For example,
    direct filtration without chemical pretreatment can
    result in a significant health risk to the consumers.
    The  Filter 6 effluent  turbidity  plot  presented  in
    Figure 4- 30  is  from a special  CPE study and
    indicates  that the  coagulation process  has  not
    been  optimized.

 2.  Disinfection - Design: The limited volume of the
    clearwell  results  in  inadequate chlorine  contact
    time,  which  in turn limits the time the chlorine has
    to  act on pathogenic organisms  that may have
    passed  through  the previous treatment  process.
    There was also an  inadequate free  chlorine
    residual in the finished water leaving the plant.

 3.  Sludge  Disposal  -  Design:  No sludge  disposal
    facilities exist to treat the sludge generated in the
    water  treatment process. The city is  in violation of
    the State Clean Water  Act  because  of the
    discharge of sludge to the river and has hired  a
    consultant to evaluate the  problem and design  a
    remedy.

 Factors identified as having either a minimal effect on
a routine  basis,  or a  major effect on  a periodic basis
were prioritized and are  summarized below.

 1.  Process  Flexibility  -  Design:  There  are  no
    provisions  for   chemical  feed  to  the pre-
    sedimentation basin or to  the  filter influent.
    Addition of these chemical feed  points would allow
    operators to better control finished water quality.

2.  Process Control Testing - Operation:  The absence
    of  or  the wrong  type  of process control testing
    results in  improper  operational  control decisions.
    The solids contact unit should be monitored more
Figure 4-29.  Plant 6 direct filtration results, February 1988.

  Finished Water Turbidity, NTU

    2.5  i-
    2.0
    1.5
    1.0
    0.5
             Proposed Finished Water MCL
         J	I
                    5            10          15

                     Day of Month
Figure 4-30.  Plant 6 effluent turbidity after backwash,
           September 21,1988.

 Turbidity, NTU                            ,
                 Proposed Finished Water MCL
   0.4  -
   0.2
       	I
J	I
I	I
I    I
              20
                      40       60

                      Time, min
                          90
                                                   51

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Figure 4-31.  Plant 6 turbidity.
                95% Compliance
                with 0.5 NTU
                  Jul   Aug  Sep   Oct  Nov  Dec   Jan   Fed  Mar  Apr  May   Jun   Jul
                  87    87    87   87    87    87   88   88    88    88    88   88    88

                                                    Date
    thoroughly and more frequently. Sample taps and
    continuous monitoring turbidimeters should  be
    installed  on each  filter effluent  so that discrete
    changes  in filter  performance may be  observed
    before substandard  quality water  is produced.
    Process control activities should be integrated into
    the daily routine of operation.

3.  Solids Contact Unit - Design: The solids  contact
    unit severely limits flow during peak periods when
    the surface overflow rate becomes excessive, and
    results in a high solids loading to the filters.

4.  Planning  and  Guidance - Administration: More
    emphasis should  be placed on  ongoing capital
    improvement  and  replacement  of equipment.
    Long-term reliability  of the  plant has been
    jeopardized by a  reluctance  to  make  necessary
    expenditures.  Administration  should develop  an
    integrated approach to setting goals, not only for
    maintenance  and  process control, but also  for
    meeting minimum finished water quality goals and
    sludge discharge limitations.

In  addition  to  the above  major  factors  limiting
performance,  other factors  identified  as  having a
minor effect were  noted during the evaluation.  Overall,
there is a heavy focus on maintenance at the expense
of adequate process control. Action taken to  address
these  factors may not  noticeably improve  plant
performance, but may improve the efficiency of plant
operation:

•  The screens  on the raw water  pumps plug with
   moss at  certain times of  the year.  Cleaning  the
   screens  is very labor  intensive. Frequent plugging
   of the screens affects water  quantity more than
   finished water quality.

•  If filter aids are used to improve filter performance,
   it may be necessary to agitate the filters by hand
   during backwash to facilitate cleaning. This practice
   will be rather labor intensive.

Projected Impact of a CCP
The evaluation   team believed that  a CCP that
addressed factors related to plant operation,  such as
operator  application of  concepts,  process control
testing, and flexibility could improve plant performance
for the majority  of the  year.  However,  continuous
compliance  with  proposed  regulations  for  finished
water  turbidity  and  disinfection, and  with  existing
NPDES permit limitations on  sludge  discharge  to the
river, would require design modifications as well.
                                                   52

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Plant 7

Facility Description
Plant 7 is  a conventional plant that treats water from a
river for industrial and  domestic use by the city. The
peak day  demand for a 12-month period was 202 Us
(4.6 mgd) based on plant records. Plant 7 includes the
following unit processes (see Figure 4-32).

•  Concrete  river  intake structure  that  houses
   manually cleaned  bar  screens, 1.9-cm (3/4-in)
   spacing.

•  Three  manually  operated  raw water pumps: one
   turbine  - 126 Us  (2,000 gpm), and two centrifugal -
   126 Us (2,000 gpm)  and 88  Us (1,400 gpm)

•  Three  turbine  pumps  used  to  pump  raw  water
   directly to a large refinery;  one 76 Us (1,200 gpm)
   and two 126 Us (2,000 gpm)

•  46-cm  (18-in) Parshall flume used to monitor raw
   water influent flow

•  Liquid alum feed pump with a backup dry alum feed
   system

ซ  Polymer feed pump

•  Fluoride feed system for sodium silica fluoride

•  Six manually-cleaned, uncovered "hydraulic"
   flocculation  basins  ("mud  basins"), each with  a
   volume of approximately 81,400 L (21,500 gal)

•  Two manually cleaned  sedimentation basins, one
   covered and  one uncovered. Each  basin  has  a
   volume of approximately 2.8 million L (750,000 gal).
   Basin effluent is transferred to the filters through  a
   61-cm (24-in) pipe

•  Two 8.5-m x 7.6-m  (28-ft x 25-ft) mixed media
   filters

•  Gas chlorination system

•  Two filtered water "transfer"  pumps controlled by
   an altitude valve  that "transfer" filtered  water to  a
   standpipe or to the high-service pumps

o  On-site  standpipe with  a capacity of approximately
   94,625  L (25,000 gal)

•  Five high-service centrifugal  pumps:  two 157  Us
   (2,500 gpm), one 126 Us (2,000  gpm), one 63  Us
   (1,000 gpm), and 38  Us (600  gpm)

*  Sludge  holding lagoon  of approximately  3.4 million
   L (900,000 gal) capacity

•  On-site  storage of sludge from the holding lagoon
 River  water  is  drawn  from  the  concrete intake
 structure  located in the middle of the river through
 41-, 36-,  and 51-cm  (16-, 14-, and  20-in) lines.  The
 intake  structure is  modified during winter months to
 include a perforated culvert intake, which  lessens the
 impact  of pack  ice. A portion of the raw water from
 the  intake structure  is  pumped directly  to a  local
 refinery.

 Raw water pumps located in a pump station adjacent
 to the plant  deliver the  desired volume of water for
 treatment. The  operators indicated  that  the turbine
 pump is unable  to achieve rated capacity  output.  The
 pumps  discharge to a Parshall flume. At  the time of
 the CPE,  sodium silica fluoride and  liquid  alum  were
 being added just upstream of the throat of the Parshall
 flume.  The superintendent had only recently switched
 from dry to liquid alum. Historically, polymer had  also
 been added at the flume location.

 After the flume,  the water flows to the "mud basins,"
 a series of six tanks used for flocculation. The basins
 appeared  to be  functioning well even though the  only
 energy  impact was  that generated hydraulically.   The
 operators  indicated that observing the floe formation in
 these basins  was  critical in  adjusting  the chemical
 dosages to the raw water. These basins are not used
 in  the  winter because of icing problems.  The basins
 have noticeably  deteriorating  concrete, and  a
 consultant had been  retained  to  evaluate their
 structural  integrity.

 From the  mud basins, water flows in  series through
 two manually cleaned sedimentation  basins. The  first
 basin is uncovered and  is used only during  warm
 weather months. During winter operation, the covered
 basin is used for both flocculation and sedimentation.
 The basins  are cleaned  manually approximately six
 times each year, and the sludge is  pumped to the
 earth sludge holding pond; 3-6  hr  are required to
 clean the  basins, and no routine sampling is done on
 them.

 Effluent from  the covered  sedimentation  basin is
 collected in a 61-cm (24-in)  pipe and delivered to the
 mixed-media  filters.  The filtration rate is controlled by
 a transfer pump located  at  the discharge from each
filter. The transfer pump discharges  filtered water to
the distribution headers of the high-service pumps  and
to  an on-site  standpipe. The transfer pumping rate is
controlled  by  demand and by an  altitude valve which
 receives a signal from a pressure sensor on the on-
site standpipe.  This filter  control has been set to
respond relatively slowly so  as  to  minimize  rapid
fluctuations in filtration rate.

 Backwash consists of a surface wash  and gravity
backwash using  the water stored  in the standpipe. At
the time of the CPE, filter runs were approximately 10-
20 days, and  a dirty filter was started and  stopped on
a daily  basis.   Backwashing  was  intended to be
                                                  53

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Figure 4-32.  Plant 7 process flow diagram.
Flocculntion
   Basins
                   Sludge Holding
                      Lagoon
                       Filter
                                    Sedimentation
                                        Basin

                                     (uncovered)
                                    Sedimentation
                                        Basin
                                       (covered)
Filter
       Transfer
       Pumps
                                              C12
                     To Distribution System       I
                                                                                                                Standpipe
                                                             a
                            a
                                           High
                                           Service
                                           Pumps
                                                                                                                 River
                                                              54

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  initiated when the headless exceeded 2.4-2.7 m (8-9
  ft) or  the  effluent  turbidity  exceeded  0.5  NTU.
  Backwash water was directed to the sludge  holding
  pond.

  After filtration, the plant effluent is chlorinated and
  pumped by the high-  service pumps to the distribution
  system. The plant does not have a clearwell  to allow
  contact  time of the  chlorine  with the treated water,
  and the first consumer is located  approximately 275 m
  (300  yd) from  the  plant  site.  The target  chlorine
  residual  is 0.7-0.8 mg/L

  Operators attempt to  match water demand with high-
  service pumping. However, caution is used in turning
  on high-service pumps so as to avoid high pressure in
  the distribution system.  Excessive system pressures
  have resulted in  broken lines because of the existence
  of old pipes in the  system.  The 38-L/s  (600-gpm)
  high-service pump was out of service at the  time  of
 the CPE.

 Sludge  from  the sedimentation basins and the filter
 backwashes is stored in the unlined sludge  storage
 lagoon from which it is dredged approximately every 2
 years and stored in  a  ditch  adjacent to the  lagoon.
 Supernatant from the  lagoons is pumped back to the
 head of the plant.

 Dried  sludge is removed from the  ditch and stockpiled
 on the  plant side.  Present stockpile volumes  have
 practically filled  the available space, and  alternative
 disposal  options  will be necessary in the foreseeable
 future.

 Operation is  almost  totally  manual. Pump settings,
 chemical dosage rates,  and filter  backwashing are all
 initiated  manually by the plant operators. The  plant is
 staffed 24 hr every day with four operators  rotating
 shifts every 28 days. A relief operator is available.

 Major Unit Process Evaluation
 The performance potential graph is shown in Figure 4-
 33. The  flocculation basins  were  rated  based on a
 detention time of 40  minutes,  which resulted  in a
 capacity rating of approximately  206 Us (4.7 mgd).
 The 40-minute detention time  rating  is  relatively
 conservative  but is  justified  because   mechanical
 mixing is not  provided.  This rating is slightly  higher
 than the  current peak  demand;  therefore, the unit
 process is deemed satisfactory.

 The sedimentation basins were rated on  a hydraulic
 loading  rate of 12  m3/m2/d  (300  gpd/sq  ft )  and a
detention  time of  5.4 hr because of the relatively poor
outlet structure (e.g.,  a  61-cm [24-in] pipe) and the
absence  of mechanical sludge  removal.  Polymer
addition  was assumed  in establishing  this  rating.
Based on these criteria,  the   capability of  the
  sedimentation  basins was assessed  as 263 Us (6
  mgd).

  The  mixed media  filters  were assessed based on  a
  filtration rate  of  293 m3/m2/d (5 gpm/sq ft). At  this
  rate, a potential capacity of  438 L/s (10 mgd) was
  projected for the existing filters.

  Disinfection capability was severely limited based on
  current state  criteria of  a 2-hr  detention time after
  chlorination.  A  capacity  of 11  L/s  (0.25 mgd)  was
  projected  based on  the  2-hr  standard and  the
  approximation that there are 274 m (300 yd) of 36-cm
  and 41-cm (14- and  16-in)  pipes  prior to  the first
  system user. Despite revisions of existing regulations
  that may allow lower detention times, the absence of
  any clearwell or contact basin  will  remain a  unit
  process limitation.

  Except  for  the  noted  limitation  in  the  disinfection
  process, unit processes were assessed adequate to
  meet the current peak demand of 202 L/s (4.6 mgd).

  Performance Assessment
  In general, the CPE indicated that a high quality water
  (e.g., turbidities  less than  0.15 NTU) was produced.
  However,  some difficulty  with  performance  was
 indicated during  winter operation. Figure 4-34, which
 shows a plot of  filter turbidity  and headloss vs. time,
 indicates an  excessively  long recovery time  after
 backwash of Filter 1 (e.g., 36 hr until effluent turbidity
 stabilized).  Ideally,  performance  stability  would  be
 achieved in less  than  10 minutes.  Also shown is a
 period of approximately 12 hr in which  the  turbidity
 exceeded  the  current state criteria of 1 NTU. Cold,
 low turbidity, low  alkalinity water and use of only the
 covered sedimentation basin may have contributed in
 part  to  the  noted  difficulties. Greater operational
 control and perhaps additional chemical  conditioning
 may be required to improve performance.

 Another  problem  indicated on Figure  4-34 is the  time
 of  deteriorated performance before a filter backwash
 was implemented. Turbidities  increased  from  the 0.1
 NTU range to the 0.35 NTU range, and approximately
 1 full day  passed before the operators  initiated
 backwash. Failure to backwash when turbidity  begins
 to  increase can  allow  significant breakthrough  of
 particles, causing a  potential health  risk for the
 community.  Figure 4-35  shows March  1989 turbidity
 data for Filter 2 with results similar to those in  Figure
 4-34. The performance problem indicated on Figure 4-
 35, however, is much more severe. Initial turbidities,
 after filter startup, exceeded the  state requirements
 (1.0 NTU)  for over a day.  Additionally, backwashing
 was delayed for approximately 3.5 days from the time
 indicated by plant data. Proper chemical conditioning
and closer attention  to the need to backwash  would
have  lessened   the  potential  for  health  risk
demonstrated by these data analyses.
                                                   55

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Figure 4-33. Plant 7 performance potential graph.


    Unit Process
               Flow, mgd
             4          6
                                                                                         10
                                                                                                      12
    Flooculatlon1
      Detention time, min


    Sedimentation2
      SOR, gpd/sq ft

      HOT, hr


    Filtration
      HLR, gpm/sq ft



    Disinfection3
      Contact time, min
 93
            46
100
            200
16.2
            8.1
                       3(
                                                      Actual Max. Day
                                                        5/88 - 4/89

   1 Ftocculation basin rated at 40-min HOT because there is no mechanical mixing.
   2 Rated at 300 gpd/sq ft and 5.4 hr because there is a poor outlet and no sludge collection equipment. Assumes polymer use..
   3 Based on current State standard of 2-hr HOT. Assumed 300 yd of 14- and 16-in pipe to first user. Standards are being revised and
    lower detention times may be allowed for existing plants.
During the CPE, a special study on filter startup was
conducted  under spring runoff  water  conditions.
During the study, Filter 1  was removed  from service
for backwashing and  Filter 2 was  placed  in service.
The results  of this analysis showed  that  turbidities
never exceeded  0.15  NTU during and  after startup of
Rlter 2.  The  stability  of the filter's performance was
also demonstrated when  the flow  was increased
dramatically  over  a  short  period  of time and no
increase  in  turbidity  occurred.    An  additional
evaluation of the surface of Filter  1 after  backwash
revealed  no mudballs, indicating that the  backwash
procedure was adequate.

Performance-Limiting Factors
The following factor was identified  as  having a major
adverse  effect  on  performance  on a  long-term
repetitive basis.

1.  Disinfection - Design: A detention  time of  2 hr is
    not  available at  the  plant  to ensure effective
    disinfection of the treated water prior to use. The
    new  regulations that  will  be  promulgated as  a
    result of  the SWTR and/or current  state  criteria
    may necessitate capital  improvements in order to
    provide  adequate disinfection capability.  This
    factor was asterisked because the final rule and
    direction could not be established until the latter
    part of 1989.
             Factors identified as having either a minimal effect on
             a routine  basis, or a major effect on a periodic basis
             were prioritized and are summarized below:

             1.  Supervision/Staff  Morale  -  Administrative:
                 Communication between administrative personnel
                 and the plant staff, and communication among the
                 staff is limited and  strained. As  a result of the
                 limited communication;  data  interpretation,
                 initiative,  maintenance efforts,  proper  process
                 adjustments, understanding of standard  operating
                 procedures, and "cross training" of personnel are
                 limited.  The operators  seem to  function
                 independently on  each  shift.  This limited
                 interaction is  believed to  be a major  contributing
                 factor to the poor  operational  decisions that
                 resulted in  the deteriorated filter  performance
                 documented  in  Figures  4-34  and  4-35.
                 Administrative skills and operator attitude will have
                 to be  addressed to eliminate the impact of this
                 factor.

             2.  Application  of Concepts  -  Operation: Inability  to
                 apply  proper  concepts to optimize unit process
                 performance  was identified  for  several  reasons.
                 First  the  supervision/staff morale  problem  limits
                 the capability of current personnel to learn from
                 each  other and, therefore, limits their  capability to
                 properly and consistently  apply  basic  concepts to
                 operational  decisions. Also,  the  practice  of
                                                     56

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 Figure 4-34.  Turbidity and headloss profiles for filter 1 - Plant 7.
_g
•a
CD
I


as
&
jg
n
                                                                                                            Headloss
                                                                                                           Turbidity
                                                  February 1989
Figure 4-35. Turbidity profile for filter 2 - Plant 7.
ZD
>;
.*=!
•o
•e
1 .5 	 ซ_ 	
1.4--
1.3 -
1.2 -
1.1 -

0.9 -1
o.a -
0.7 -
0.6 -
0.5 -
0.4--
0.3 -
0.2 -
0.1 -
0 -



I
] Current Standard
—

I Recommend f
I initiate 	 5 	 f-
	 41 	 	 — 	 	 Rfirkwash a J Wi

\ \ 1 jf^V
\A • / W
fijTS U* J%i ~" 	
1 ™ FWI T r
Wy^^^E^ js^ _ jiT ^TB
anrtr>- cyry 	 	 . 	 _
. • • • 	 ' 	 	 i • ••••" 1 1 ' 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1
11 12 1314- 15 16 17 18 19 20
                                                 March 1989
                                                        57

-------
    routinely starting up a dirty filter and of occasion-
    ally  "bumping" the  filters with large changes  in
    flow rate can and has resulted in  turbidity  spikes
    and the associated  breakthrough  of  particles.
    Particle breakthrough represents a high potential
    health risk.

3.  Policies  -  Administration: The implementation  of
    very tight fiscal policies limits the expenditure  of
    funds  for  necessary items. The  lack  of  in-line
    turbidimeters for  the two  filters,  an  additional
    polymer feed  pump, and use  of polymer  was
    assessed to be impacting plant performance. The
    CPE did  not identify where these  policies were
    originating.  It  was  felt  that improved
    communication would greatly assist  in addressing
    this factor.

Chemical  feed capability was identified as  having  a
minor  impact  on  performance.   Moving  the
alum/coagulant feed point from  its present location to
the throat of the Parshall flume would allow a better
rapid mix to occur and may result in lower chemical
use. As a side benefit, the raw water sample could  be
taken in the chemical feed  room, although the  sample
would contain fluoride.
Projected Impact of a CCP
Generally, the  plant was producing a  high  quality
treated water. As such, a CCP would not dramatically
improve water quality.  However, intangibles such as
communication, operational concepts, and  a "tight"
fiscal policy represent deep-seated problems that may
be difficult to address using past practices. From this
point of view, an external facilitator may be necessary
to impact the current situation.

In lieu  of  a CCP,  it  was recommended that the
community pursue a correction effort to address the
factors  identified  as  limiting  plant performance,
recognizing that  they will be difficult  and  time
consuming to eliminate.
                                                    58

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 Plant 8

 Facility Description
 Plant 8,  operated by  the county  sewer and water
 district, treats water from  a nearby  river for domestic
 use by the town and a local  rural water system. The
 plant, which began operation  in 1981, utilizes a solids
 contact  clarification/filtration  process.  Extreme
 variations  in turbidity exist in  the  river.  During  the
 winter, turbidity is generally below 30 NTU  and can  be
 as low  as 10  NTU;  however, during spring and
 summer,  turbidity ranges from 40 NTU to as high  as
 several thousand  NTU  as the result of storm events.
 Plant  8  includes  the following  unit processes  (see
 Figure 4-36).

 • 1.2-m (4-ft) diameter  corrugated steel intake which
   extends  below  the river bottom.  The steel intake
   pipe is  perforated and  packed with gravel in the
   area below the river bottom

 • Wet well with  two 16-L/s  (250-gpm) submersible
   raw water  pumps.  The pumps  are  automatically
   operated from a level signal in the plant clearwell.

 • 15-cm (6-in) diameter propeller meter for measuring
   the raw water flow rate

 • 110-4,375 kg (240-9,645 lb)/d dry  alum feeder

 • 3-15 L (0.1-0.5 cu ft)/hr lime feeder

 • 3-15 L (0.1-0.5 cu ft)/hr soda ash feeder

 • Polymer feed system  with a 170-L (45-gal) dilution
   tank and  a 3.7-20.8 L (1- 5.5 gal)/hr feed pump

 •  Steel, 5.5-m (18-ft) diameter, 3.2-m  (10.5-ft) deep
   solids contact unit with 45ฐ tube settlers

 •  1.3-6.8 L (0.34-1.8 gal)/hr polyphosphate  feeder

 •  11 -kg (24-lb)/d carbon dioxide feed system and an
   associated in-line static mixer

 •  Steel 3.2-m (10.5-ft) diameter  dual-media filter

 •  9-kg (20 lb)/d gas chlorination  system

 •  56,000-L  (14,800-gal) clearwell with  baffled
   compartments

•  Two 16-L/s (250-gpm) vertical turbine pumps which
   pump treated water to the distribution system and  a
   storage tank

•  Two sludge holding lagoons with a total capacity of
   approximately 658,200 L (173,900 gal)

•  Spent  backwash storage lagoon  of approximately
   2.1  million-L (556,170-gal) capacity
 River water  flows to the  raw water pump  wet well
 through a  pipe  that is  located inside the corrugated
 steel intake structure. The  original intake configuration
 consisted of  an  infiltration  gallery located in the river;
 however, due to plugging of the gallery with sediment,
 the  system was replaced in 1986  with the current
 intake pipe. The  operator  and  board members
 indicated that the original  infiltration  gallery  provided
 water of much  lower turbidity than the current intake
 structure. However,  as the gallery  became plugged
 with sediment, raw water capacity was reduced to the
 extent that the board decided to replace the infiltration
 gallery with the present system.

 The two raw water  pumps,  located  in  a wet  well
 adjacent  to the river, each deliver  the rated  plant
 capacity. Pump  operation is  based on a level signal
 from the  plant clearwell, and operation is alternated to
 maintain  even  run  times  on  both  units.  The  plant
 operator reported that a pump is  typically operated at
 full  capacity; however, a butterfly  valve located in the
 plant can be used  to reduce  pump capacity. In an
 attempt to  maintain  a sludge  blanket  in  the  solids
 contact unit, the operator had throttled pump capacity
 to reduce flow to the unit.  The operator felt  that this
 experiment did  not  stabilize the  process,  and since
 that time the plant has operated at 16 L's  (250 gpm).

 The  raw water  flow  rate  is indicated and  totalized
 through a propeller meter located in the raw water line
 inside the plant building. Following the flow meter, raw
 water is directed  into the  solids  contact  unit.
 Components  of  this unit  include an upflow mixing
 column with a turbine mixer, a downflow flocculation
 cone, and  an  upflow  clarifier  with  tube  settlers
 throughout the settling area.

 Water treatment chemicals  including alum, lime, soda
 ash, and polymer can be added into  the  mixing area.
 During the winter, when water hardness  increases in
 the river,  the operator can  add  lime and  soda ash to
 the  solids  contact  unit  for  softening.  During  the
 remainder  of  the year,  alum  and  a polymer  are
 typically  used for turbidity removal. The  operator
 reported that the plant  was  not operated in  the
 softening  mode  last winter and  that alum and a
 cationic polymer were used  for coagulation during this
 period.  At the time  of  the site  visit, the  operator
 indicated that 80  mg/L of alum and 2  mg/L of cationic
 polymer were being fed to the mixing tube.

 A variable speed turbine mixer located on top of the
 mixing tube directs the  incoming  raw  water  upward
 through the tube and  out into the flocculation cone.
 The  mixing tube is open at  the  bottom, thus allowing
 the recirculation of flocculated water with the incoming
 raw  water. The  amount  of  recirculation depends on
the speed of the turbine   mixer.  According  to the
operator, the turbine mixer speed  has been operated
throughout the entire  range,  without changing the
performance characteristics  of the solids  contact unit
                                                  59

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Figure 4-36.  Plant 8 process flow diagram.
                    River
                                   Raw
                                   Water
                                   Pumps
   Flow
   Meter
                                                                             Backwash
                                                                              Supply
                                                                               Line
                                    Solids
                                 Contact Unit
   Sludge Beds
                                       Alum, Lime,
                                       Soda Ash,
                                       Polymer
                                                                                                               Backwash
                                                                                                                Control
                                                                                                                 Valve.
                                                                                      Clearwell
                                                            Filter Rate
                                                            Control Valve
High
Service
Pumps
                                                                                                                 To
                                                                                                             Distribution
                                                                                                               System
                                                           60

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except at high  speed.  At high  speeds,  turbulent
conditions in the unit degraded clarifier performance.
The current  practice is to operate the turbine at low to
medium speed, and  the turbine and  sludge scraper
continuously, even  when the  plant is not  treating
water.

Following  the mixing tube,  the  conditioned  water
enters  an  inverted cone where flocculation occurs. At
the bottom  of  the  flocculation  cone,  water  moves
outward into the clarifier and, theoretically, through a
developed sludge blanket.  Water  then  flows  upward
through 45-degree tube settlers before  overflowing a
peripheral weir. The operator reported that he has had
a  difficult  time  controlling the sludge  blanket in the
solids  contact  unit.  It  appeared that  sludge  solids
generated in the process are typically  lost over the
weir and deposited on the filter.

Excess sludge generated in the process  can  be
directed to  two sludge  lagoons  by opening a sludge
blow-off valve. The operator indicated  that sludge has
never  been removed from the two sludge lagoons
since  startup of the  plant. Effluent from  the solids
contact unit flows onto a dual-media filter. If the plant
is operating  in the softening mode, carbon dioxide can
be added for pH adjustment after the solids  contact
unit. Mixing  is accomplished by an in-line static mixer.
Polyphosphate  can  also be added at this location to
control calcium carbonate  buildup in  the filter.  Even
though the  plant was not  operating in the softening
mode  during the site visit, polyphosphate was still fed
to the  solids contact unit effluent.

Water  level  in the filter is controlled by a modulating
flow control valve. According  to  the  operator  and
several board members, this control valve has never
provided  a  constant-rate operating   condition  as
intended  by the  original  design.  Until  just  recently,
water  level  in  the filter would  fluctuate dramatically
during a  filter run,  causing sudden,  high  magnitude
flow rate changes through the filter. This condition has
improved  significantly since the plant operator and a
board  member fabricated an adjustment mechanism to
control the travel distance of the valve seat.

Backwashing of the  filter  can  be initiated  by either
filter headloss or filter effluent turbidity. The backwash
supply water is  provided  by  the  pressurized
distribution system including an elevated storage tank,
and the backwash rate is controlled  by a  pressure
reducing valve. Spent backwash water is directed to a
storage lagoon  located adjacent  to  the plant.  The
operator reported  that  spent backwash water seeps
into the ground water and has never accumulated in
the lagoon.

Treated  water  from the filter  is chlorinated  and
directed to a baffled  clearwell. The two vertical turbine
pumps deliver treated water to the distribution system.
Pump operation is based on a  water level signal from
the  elevated  storage  tank. When  operated  in
automatic mode, the plant may start and stop more
than once daily  with each start  on a  "dirty" filter.
According to the operator, the  clearwell is taken out of
service  once  each  year to  remove  accumulated
sediment in the tank bottom.

Operation  is usually by  the  automatic  mode (i.e.,
storage  tank elevation).  During  peak water  usage
periods in the summer months, the plant operates 12-
14 hr each day at the design rate  16  Us (250 gpm).
Less operating  time  is required during the winter. The
plant is staffed about 2-3 hr each day by one operator.
Board  members assist with  plant maintenance and
repair  on an as-needed basis. The plant operator is
also responsible for a  booster pump station  and
distribution system serving the rural water members of
the district. The operator and board members reported
that maintaining this part of the system can be  very
time consuming because  of frequent leaks that occur
in areas of the rural distribution system.

Major Unit Process Evaluation
The performance potential graph is  shown in Figure 4-
37. Mixing, flocculation, and sedimentation processes
all  occur  in  the  solids  contact  unit.  Although
flocculation is typically evaluated on the performance
potential graph, it was not included here because the
process  occurs  within   the  solids  contact unit.
Flocculation in  solids contact units is enhanced by the
recirculation of  flocculated water  through the  mixing
tube with the incoming  raw water.  The sedimentation
component of  the solids  contact unit  was rated at a
surface overflow rate of 58 m3/m2/d (1,421 gpd/sq ft),
which  is slightly less than the design rate. This rating
is also based on incoming raw water turbidity levels of
less than 500  NTU, which is typical for most of the
year, and a relatively shallow depth of 3 m (10  ft). For
occasions when turbidity is greater  than 500 NTU, the
sedimentation  component was rated  at a  surface
overflow rate of  32  m3/m2/d (790 gpd/sq ft) or 8 L/s
(125 gpm). At this turbidity level, control of the sludge
blanket might be difficult and solids loss from the unit
would begin to  affect  filter performance.  The plant
could  overcome this  limitation by operating  at  the
lower  flow rate  of  8  L/s (125 gpm) over a longer
period of the day.

The dual  media  filter  was assessed  based on  a
filtration rate of  176 m3/m2/d (3  gpm'/sq ft).  At  this
rate, a  potential capacity of  16  L/s (250  gpm) was
projected for the existing filter. In  some  cases, dual-
media filters have been  rated over  176 m3/m2/d (3
gpm/sq ft); however,  because of  the  complex
operations associated with the solids contact unit, a
conservative filtration rate was selected.  This rating
also assumes  that the existing effluent control valve
limits extreme variations in water flow rate through the
filter. Although the modifications made to the  control
valve  appear  to  have  significantly  improved  filter
operation, adequate time was not available during the
                                                   61

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Figure 4-37. Plant 8 performance potential graph.


    Unit Process
                                          50
   Flow, gpm

100         150         200         250
                                                                                                   300
Solids Contact Unit1
SOR, gpd/sq ft
Filtration*
HLR, gpm/sq ft
Disinfection
Contact time, hr


316 632 947 1,263

0.6 1.2 1.7 2.3 2

4.9 2.5 1.6 1.2 1




9

0

                                                                                       Design
                                                                                        Flow


   1 Capacity reduced to approximately 125 gpm when turbidity >500 NTU. Shallow,  10-ft deep clarifier limits capacity to  <250 gpm
    when turbidity >500 NTU.
   2 Assumes adequate filter effluent control valve.
site visit to  thoroughly  evaluate  the  valve's
effectiveness.

The chlorine contact basin was rated at 16  Us (250
gpm) based  on a hydraulic  residence  time  of 1  hr.
Disinfection capability  is  typically based on current
State  criterfa  of  a  2-hr  residence time  after
chlorination. The 1-hr residence time was allowed in
this case because of the efficient baffling that exists in
the contact basin.

At the present time, the plant operates at the  16  Us
(250 gpm) rate for about 12-14 hr/day during  the peak
demand  period.  The  performance potential  graph
indicates that this peak demand can be met when raw
turbidity  is  less  than  500  NTU  without significant
changes in hours of operation.  To  meet  the peak
demand when turbidity  is  greater  than 500  NTU,  the
plant would  have to operate  at  a  reduced rate  of
approximately 8 Us (125 gpm) over a 24-hr period.

Performance Assessment
This plant has historically had  operational  problems
associated with the operation of  the solids contact
unit. During  the CPE  site  visit,  the  plant  operator
reported that maintaining a sludge blanket in the solids
contact unit has been a problem since startup. Other
operations-related information obtained during the site
visit indicated that performance problems have been
more common  than  indicated  by plant monitoring
reports. Rgure 4-38 shows  the number of days that
treated water turbidity exceeded 0.5 NTU (the  SWTR
turbidity standard for treated surface  water)  for each
month over the past year. This analysis indicated that
performance problems  have occurred on a  frequent
 basis over the past year, and have been more severe
 during the winter months  when  low turbidity,  cold
 water was treated by the plant.

 During the CPE, a special study on filter startup under
 two  different  conditions  was  conducted.  The  first
 condition  consisted  of starting a  dirty  filter  (i.e.,  a
 condition  in  which  a backwash  had  not occurred
 before filter startup) and  monitoring effluent turbidity.
 The  operator indicated  that  this condition  occurs
 routinely at the plant  because of the automatic mode
 of operation.  A graph of filter  performance under this
 condition is shown in  Figure 4-39.  As shown, following
 filter startup effluent turbidity immediately increased to
 over 5  NTU  and then gradually decreased  to about
 1.5 NTU after 20 minutes. Results of this test indicate
 that  starting  a  dirty  filter results  in turbidity levels
 above the 0.5-NTU  limit for  an  extended period  of
 time and presents a significant  danger of  passing
 pathogenic organisms through the  filter.

 The  second  condition of the special study involved
 backwashing  the filter and monitoring  the  effluent
 turbidity after it was  placed  in operation. As shown in
 Figure  4-40,  turbidity after   backwash  increased
 immediately to a peak value of 13.5 NTU. About 25
 minutes  after the  filter startup, the  effluent  turbidity
 decreased to  the 0.5-NTU  level.  This condition  also
 indicates  the  potential  for  pathogenic  organisms  to
 pass  through the filter.  Properly  conditioned filters
 typically experience a turbidity  spike of less than 0.2
 NTU for less than 15 minutes.

 Several  problems  associated  with the  backwash
 contributed to  the  subsequent  poor performance  of
                                                   62

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  Figure 4-38. Plant 8 performance.
              Jun     Jul    Aug    Sep    Oct    Nov    Dec    Jan    Feb    Mar   Apr   May
 the filter. When the backwash sequence was initiated,
 the surface wash valve did not open. According to the
 operator,  the surface wash normally operates  the
 entire  length of the backwash  period. The filter was
 washed for  over  23 minutes,  a  much  longer than
 normal duration for this function, without getting clean.
 Because  of  the  dirty  condition  of the filter,  the
 backwash  rate was  manually increased by adjusting
 the control valve, but never succeeded in cleaning the
 filter. Measurements of the rise  rate in the  filter at the
 beginning  of  the backwash indicated a backwash rate
 of approximately 645 m3/m2/d  (11  gpm/sq ft), less
 than the   minimum  recommended  value of 878
 m3/m2/d  (15  gpm/sq ft).  Proper adjustment  of  the
 backwash  control  valve would allow an  adequate
 backwash flow rate.

An additional  factor that  could have  contributed to the
plant's poor  performance during  the CPE site visit
relates to the alum feed  rate  to the solids contact unit.
The operator  indicated that the  alum feed 'rate  to this
unit was approximately  80 mg/L. Upon checking  the
alum feeder  by  weighing  a sample of dry  alum
collected   over  a  selected time  period, it  was
determined that the actual alum feed rate  was  about
177 mg/L.  Since the  raw water turbidity was about 80
NTU at the time  of the site visit, alum was probably
being overfed at this dosage rate. Following  further
investigation into this problem, it was determined that
the operator had exchanged the alum feeder with the
lime feeder. This change was implemented so that the
feeder with a vibrator could be used for lime addition.
The operator was not aware that the new alum  feeder
had a 3.8-cm (1.5-in) feed screw instead of a 1.9-cm
(3/4-in)  feed  screw,  thus  causing a  higher-than-
expected alum dosage.

Performance-Limiting Factors
The factors identified as  having a major  effect on
performance on a  long-term  repetitive  basis  were
prioritized and are summarized below:

1-   Water Treatment Understanding - Operation: Lack
    of operator understanding of water treatment has
    been a  major cause of the performance problems
    experienced at the plant. The plant operator never
    received any formal training on operation of the
    plant. This situation  is  compounded  by  the fact
    that  the solids contact process is  complex and
    requires a high level of process control to achieve
    good performance.   Examples of  this  lack of
    understanding include  incorrect calculations of
                                                  63

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Figure 4-39.  Turbidity profile - dirty filter startup - Plant 8.

 Effluent Turbidity, NTU

  6   r-

0

1
5

1
10
Time, min
I
15

I
20

  jure 4-40. Turbidity profile - filter startup after backwash
           Plant 8.

  {fluent Turbidity, NTU

    14
     4  ~
      2  -
               5      10      15

                       Time, min
                                     20
                                             25
    alum and polymer feed  dosages, startup of dirty
    filters, inadequate process control testing, and an
    inadequate filter backwashing procedure.

2.  Process Control  Testing - Operation: The current
    process control  testing  in  effect at the plant  is
    inadequate.  The only  process  control testing
    currently done is periodic jar testing to determine
    chemical  dosages.  Jar testing should  be
    completed whenever  raw water quality changes
    significantly.  Control of the solids contact  unit
    requires daily  monitoring of influent and effluent
    turbidity,  sludge  blanket  concentration  and
    location,  and  blowoff  sludge   volume  and
    concentration.  The plant does  not  have adequate
    testing equipment to perform many of these tests.
    Although a jar  testing apparatus is available at the
    plant,  it does  not  accurately  simulate  the
    flocculation and coagulation processes.  Equipment
    necessary to  monitor  the solids contact  unit
    includes a blanket finder and a  centrifuge.

3.  Plant Coverage - Administration:  Paid coverage  at
    the plant is presently 2- 3 hr/day, 7 days/week. If
    unanticipated  problems  develop at the plant  or
    distribution system  that require  time beyond the
    routine amount, the operator and board members
    volunteer  time  to  correct the  situation.  The
    operator's  son  currently  acts  as   a backup
    operator; however, he has not received  any  formal
    training and is not certified  in  water  treatment.
    Given  the complex nature of the  plant and the
    potential  for  extreme  variations   in   raw  water
    quality, coverage  at  the  plant  needs   to  be
    extended. Ideally,  whenever the plant  is  in
    operation, an  operator  should  be at  the  plant
    monitoring its  performance. A minimum of 4  hr
    each day probably  would be required  to perform
    routine process control testing,  data analysis,
    reporting, and preventive maintenance activities.
    Realistically, it would  probably be  difficult to  staff
    the plant at all times that it is in operation because
    of the  small  size of  the district. A possible
    compromise  could  include  increasing  plant
    coverage to  a minimum of 4 hr/day, not including
    the distribution system, and adding an alarm/dialer
    system at the plant.

4.  Insufficient  Funding/Bonded  Indebtedness  -
    Administration: The district received  a 40-year
    loan from the  Farmer's Home  Administration  to
    fund  the  construction of  the  plant  in  1981.
    Repayment of this loan  requires approximately  50
    percent of the district's revenues at the present
    time.  Because of the small size  of the  district,
    approximately  46  town customers and 62  rural
    customers,  and the  large  indebtedness,  water
    rates  are moderately high relative  to other  similar
    systems. Rates  were recently increased to assist
    in rebuilding a  reserve  fund  that was depleted
    when the new intake structure was installed. Even
                                                   64

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    with these  moderately  high  rates, revenues  are
    marginal  to  cover the cost  of  additional plant
    coverage and minor capital improvements.

Factors identified as having either a minimal effect on
a routine basis, or a major effect on a periodic basis
were prioritized and are summarized below.

1.  Plant Staff. Number - Administration:  The plant is
    staffed by one operator at the present time,  and
    he provides coverage  7 days/week. Occasionally,
    the operator's son performs as a backup operator
    when  the operator is  not available. A trained,
    backup operator is needed at the plant to routinely
    relieve the  regular  operator. Several  of the board
    members recognized this problem and  expressed
    their concern with locating a person who would be
    willing to work on a part-time basis at the pay  rate
    they  could  afford.  The operator's   son  has
    expressed some interest  in becoming certified in
    water  treatment. Given  his work experience at the
    plant,  this option  may be worth  pursing  by  the
    district.  Another option could involve utilizing an
    interested board member  as the backup operator.
    Once  trained and  certified, the  backup operator
    could   provide  plant  coverage on alternating
    weekends and during vacations.

2.  Alarm System - Design:  An  alarm  and automatic
    plant shutdown capability  are  available  when high
    turbidity is recorded from  the filter. As is the case
    with  any type of  automation, this function  has
    failed  on occasion and high  turbidity water  was
    directed  to  the  clearwell.   This alarm function
    provides  a necessary  safeguard  against
    contaminated water  entering the  distribution
    system  and  should  be  routinely  checked  and
    maintained.  Because  of the  high  degree of
    variability in  the raw  water  source,  it  would be
    advantageous to  have a similar  high turbidity
    alarm  and automatic plant shutdown  capability for
    this  source. This  capability  could  warn  the
    operator about a change in raw water turbidity and
    allow time to adjust chemical feed dosages.

3.  Chemical Feed Facilities - Design: Because of the
    exchange  made  between the  lime  and alum
    feeders, the present alum feeder does not appear
    to have a satisfactory range to feed  low dosages
    under certain water  quality  conditions.  Since
    overfeeding alum  can detrimentally  affect plant
    performance, this  problem  will  have  to be
    corrected. The operator  may want to  investigate
    changing the feeders  back to  their original
    functions. If lime is to be fed  in the future, a  new
    shaker may be required.

4.  Process Controllability  -  Design: Since  startup of
    the plant,  the  filter effluent  control  valve  has
    caused erratic control of the water level  in the
    filter.  This rapid change in filter water level causes
    particles to pass through the filter, thus affecting
    treated  water  quality.  Recently,  a  throttling
    mechanism fabricated by the operator and a board
    member has  limited these fluctuations in water
    level. With this modification completed,  this factor
    moved to  a lower  priority; however,  replacement
    of  the valve  should still  be  considered when
    funding is available.

5.  Performance  Monitoring - Operation: During  the
    CPE site  visit,  performance  monitoring  records
    were reviewed,  and some performance problems
    were occasionally noted. However, interviews and
    special  studies conducted  during  the CPE
    revealed  serious performance  problems  at  the
    plant.  Since  records did  not accurately  reflect
    actual  plant  performance,  regulatory  agency
    reviews  were  not  able to  establish  that  a
    performance problem existed.  Accurate reporting
    would probably have resulted in pressure from the
    regulatory agency and correction  of some of the
    factors noted in  this report.

6.  Raw Water Turbidity -  Design: As noted  by the
    performance potential graph, raw water  turbidity
    above 500 NTU is projected to limit plant capacity.
    High turbidity water typically  occurs during  the
    spring through  fall,  and only occasionally during
    this period as  the  result of  runoff  from storm
    events.  The  high  turbidity problem  can most
    realistically  be handled  through  operational
    changes and  minor  expenditures  for  testing
    equipment  and  an alarm  system. If the  current
    peak demand remains the same, the plant may be
    able to treat high turbidity water by reducing the
    flow rate through the plant and operating for more
    hours during the day. If operational measures are
    not successful,  there should be added flexibility to
    direct the raw water through  a pre-sedimentation
    basin  with chemical addition  capability.  A  pre-
    sedimentation pond could be  used  as a backup
    water supply during short runoff events  or used to
    lower raw  water turbidity  during longer storm
    events.

7.  Sedimentation/Solids Contact Unit -  Design: The
    solids contact unit's capability to treat water under
    a  variety  of  conditions may  be limited by  its
    relatively  shallow  3-m  (10-ft) depth  and  high
    surface  overflow  rate.  Under these conditions,
    maintaining a sludge blanket in the  unit can  be
    accomplished;  however,  considerable  process
    control testing  and possible  adjustments to the
    plant flow rate  are  required.  The short hydraulic
    residence time  in  the  unit may limit the plant's
    capability to treat cold, low-turbidity water. Under
    cold water conditions,  chemical  reactions  are
    slower and longer  residence times  are required.
    Longer  residence  times  can be  achieved  by
    operating the plant at a lower rate for long periods
    of time.
                                                   65

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A factor identified as having a minor effect on  plant
performance  is  the  existing  chemical   feed
arrangement,  which limits  the  injection of alum,
polymer, lime,  and soda ash to the  mixing tube in the
solids contact unit. Under cold, low  turbidity water
conditions,  it  would  be advantageous  to add the
coagulation chemicals ahead of the flow meter.  This
injection location would allow more intense mixing and
slightly more detention time when  treating cold, low
turbidity water.
Projected Impact of a CCP
As indicated by the performance potential graph and
factors limiting  performance,  this  plant does have
some  design  deficiencies.  However,  operational
changes at the plant and administrative support could
be used to overcome most of these deficiencies. As
such, implementation  of  a CCP  could  demonstrate
dramatic improvement in treated water quality. Before
a CCP could be  implemented, however, the district
would  have to  commit to providing  the  additional
staffing and coverage  required to operate the plant
and  the  expenditures  necessary  to  purchase the
necessary testing equipment.
                                                  66

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Plant 9

Facility Description
Water  is supplied to the city  from four sources: a
direct filtration plant and three ground-water wells that
augment the  water  supply  during summer  months.
The  CPE was limited  to the  direct filtration plant,
which  treats  water  from an  infiltration system  for
domestic and commercial use  by  the city. The peak
day demand for a 12-month  period was estimated at
74 Us (1.7  mgd). Plant  9 includes the following unit
processes (see Figure 4-41):

• Infiltration  system  consisting  of perforated
  subsurface laterals that are  connected  to  shallow
  caissons

• 8,330-L (2,200-gal) basin that serves as a sand trap

• In-line static mixer with two elements

• 30-m2 (324-sq ft)  monomedia (sand) travelling
  bridge automatic backwash filter

• Two  polymer  feed  pumps:  one for feeding  neat
  polymer and one for feeding diluted polymer

• Gas chlorination system with two chlorinators, each
  23-kg (50-lb)/d capacity

• On-site treated water  reservoir, 33.5 m  (110 ft) in
  diameter  and  2-m  (6.5-ft)  deep (1.7 million L
  [462,000  gal])

• Propeller  meter on  the discharge  line from  the
  treated water reservoir

• On-site 12-m x 12-m x 2-m deep (40-ft x 40-ft x
  6.5-ft) concrete  backwash  holding  basin,  which
  r4ie*r*fa?3mc\o +r\ on iKKir^Qtinri Hity-*h
   discharges to an irrigation ditch
Water from one of two  creeks is diverted onto a hay
field adjacent to the  plant where the water percolates
through  several feet of  soil  to perforated  laterals
buried under the field. Water flows through the laterals
to concrete caissons,  which  are  fitted  with metal
covers.  A line  then  carries the composite  flow from
the caissons to the direct filtration  plant. Microscopic
particulate examination of the  infiltration system water
has  shown that it is directly impacted by the surface
water and, therefore,  should be considered  a surface
water source.

Raw water flows by gravity from the infiltration system
to a sand trap  basin in  the plant. Cationic polymer is
fed at the end of the basin after which the water flows
through a control valve that regulates the amount of
water treated in the plant. Any excess water from  the
infiltration system flows  over a weir  at the influent end
of the sand trap basin to an irrigation return ditch. The
control valve can operate automatically to shut down
or start the plant,  based on  the water level  in the
finished water reservoir. At the time of the evaluation,
the valve  was being operated manually to  maximize
the depth  of  treated  water  in  the  finished  water
reservoir.

After  passing  the control valve,  the  water flows by
gravity through an  in-line static  mixer  and onto the
automatic backwash filter. The filter was designed to
operate at  a filtration rate of 117 m3/m2/d  (2 gpm/sq
ft),  but was being  operated  at  approximately  211
m3/m2/d (3.6 gpm/sq ft) at the time of the CPE. The
filter has approximately 28 cm  (11 in) of sand media in
54 20-cm (8-in) sections.

The filter  sections are  separated  by fiberglass
dividers, which were warped  at the top. Because of
the warping, some  sections were only 2.5-5 cm (1-2
in) wide at the top,  while other sections were over 20
cm (8 in)  wide at the top. This variation was caused
by migration of the sand  media from one  section to
another during backwash.

The filter  can  be  backwashed automatically  by
headloss or by timer. During the  evaluation, the filter
was being  washed  automatically  based on  headloss,
with little consideration given to filter effluent turbidity.
When  the  filter  is  backwashed,  a  travelling  bridge
passes across the filter  and  washes each section.
One pump on the bridge pumps water  back  up
through the filter  section and  another pulls  the spent
backwash water from the  top of each section through
a shroud to a discharge channel adjacent to the filter.
The backwash water flows by  gravity to the backwash
storage basin.  Following  filtration,  the  water is
chlorinated  prior  to the  filter  level control  weir and
flows into the treated water reservoir. Effluent from the
reservoir flows by  gravity 8  krn  (5  miles)  to town
through  parallel  20-cm  (8-in)  and  25-cm (10-in)
transmission lines.

Sludge from  filter  backwashes  is  stored in the
concrete backwash storage basin.  Supernatant from
the basin  is discharged  over  a weir to an irrigation
ditch. According  to the operator, sludge is removed
from the basin every 3-4 years by wheelbarrow and
front-end loader and is spread  on adjacent fields.

Operation   is primarily  manual except  for  filter
backwashing.  Plant  operation, flow  rates,  and
chemical dosage  rates are all initiated  manually  by the
plant operators.  The two plant operators   spend
approximately  0.5-1 hr each day at the plant checking
the operation of the plant. During that time, the plant
is inspected  to  ensure  equipment  is  operating
properly; no significant  process  control  activities are
conducted. The operators are  also responsible for the
wastewater treatment  plant,  wastewater  collection
system, water distribution  system,  streets,  parks,
airport,  swimming  pool,   and  grave  digging  at the
cemetery.
                                                   67

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Figure 4-41.  Plant 9 process flow diagram.
                                                                                         Infiltration
                                                                                           Laterals
   Sand trap.
  Overflow
           Bypass Line
                                                                                                       Automatic
                                                                                                     Backwash Filter
                      Overflow
                                                                               To Town
                                                         68

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Figure 4-42.  Plant 9 performance potential graph.


    Unit Process
                                          0.5
               Flow, mgd

            1.0         1.5
                                                                             2.0
    Filtration1

      gpm/sq ft


    Disinfection
      Contact time2, hr

      Contact time3, hr
1.1
2.9
6.3
            3.2
                       2.1
                                                                  Estimated Max.
                                                                    = 1.7 mgd

   1 Rated at 2 gpm/sq ft because there is only 11 in of sand medium.
   2 Based on current State standard of 2-hr HOT to first tap. Assumed 10 percent volume of clearwell and 0.75 mi of 8- and 10-in pipe to
    first user. HOT refers to time it takes water to travel from the plant to the first tap.
   2 Based on current State standard of 2-hr HOT to first tap. Assumed 10 percent volume of clearwell and 2.5 mi of 8- and 10-in pipe to
    first user in town.
During the evaluation,  peak water use in the city was
approximately five times greater than typical water use
for  a community with  no large industrial users. This
extensive use required the city to augment the surface
water supply  with  three  ground-water  wells.
Determining the cause of the excessive water use and
taking measures to lower it to  normal levels  would
allow the plant to operate at lower flow rates.

Major Unit Process Evaluation
The performance potential graph  is shown in Figure 4-
42. Peak  day demand for the plant was estimated by
measuring the  depth  of flow over the filter effluent
weir and applying that  flow on a 24-hr  basis. This flow
was then  compared to projected  plant capabilities. As
Figure 4-42  shows, the monomedia  sand  filter was
assessed at  a  potential capacity of 39 Us  (0.9 mgd)
based on  a filtration rate of 117 m3/m2/d (2 gpm/sq ft).
The filter  capability was limited because a direct filter
using 28  cm (11 in) of sand cannot  be  expected to
provide consistent  performance  at rates higher than
117 m3/m.2/d (2 gpm/sq ft).

Disinfection capability  was rated based on current
state criteria of a 2-hr detention time after chlorination.
As  Figure 4-42  shows, two conditions  were  rated:
detention  time  to the  first tap downstream from the
plant and  to town. Disinfection  detention  time was
adequate  to  town  at  flow rates up to 77 L/s (1.75
mgd). However,  detention time  to the first tap only
resulted  in  a plant capacity  of  33 L/s  (0.75  mgd).
Standards are being revised and  different criteria may
be  used to allow lower minimum detention times for
existing plants,  which would likely  rely on effective
filtration.
             Because of the limitation in the filtration process, the
             plant  was  assessed  as  inadequate  to  meet  the
             projected peak demand. However,  water use on a per
             capita basis was noted to be extremely high. Normal
             water  use would  result in daily water  production of
             about  39 L/s (0.9 mgd),  which the plant should be
             able to handle on a continuous basis.

             Performance Assessment
             A review of the operating  records indicated that the
             raw water  was  of  very  good  quality with  peak
             turbidities of 0.7 NTU. Treated water was also of good
             quality with  turbidities  normally  about  0.2  NTU and
             with a peak of 0.45  NTU.  However, turbidity of very
             clear waters, such as  the water from  the  infiltration
             system,  is  often  not  a good  indication  of
             bacteriological  quality.  In fact, previous   state
             particulate  tests  revealed  that  the  filter  was  not
             removing a  significant  number of particles from the
             raw water.  The operating  data  revealed  that  only
             about 50 percent of the raw water turbidity was being
             removed.  Plant  data  taken during  periods  of no
             chemical feed and some chemical feed  indicated little
             difference  between raw  and treated water turbidity
             between the two.

             During the  CPE,  a special study was  conducted to
             determine  the effect of backwashing  the  filter on
             treated water quality. The filter was backwashed and
             samples were collected  as near  as  possible  to the
             filter cell being washed and at the filter effluent  weir.
             Figures 4-43 and 4-44  present  the  results of  the
             study. As shown, at  both sample  points effluent
             turbidity  increased significantly  (to  5  and  7-  NTU)
             during backwash  and remained above  the 0.5  NTU
                                                    69

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Figure 4-43.  Turbidity profile during and after backwash at filter effluent weir - Plant 9.
 Turbidity, NTU
     5  i-
     4   -
     3   -
     2   -
     1   -
                          Completed 1 st Pass
                                                   Completed Wash
Figure 4-44.  Turbidity profile during and after backwash at cell effluent - Plant 9.
  Turbidity, NTU
     8   i-
     7   -
     6   -
     5   -
     4   -
     O   —•
     o   •-•
     1
     0
                                                                                                                    24
                                                             70

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limit for over 60  minutes.  The study results indicate
that a significant  amount of the material removed by
the filter was allowed to pass through the filter into the
treated  water  reservoir. The  significant increase  in
turbidity is especially indicative of poor performance,
since the  raw water turbidity was only about 0.6 NTU
during the special study.

The  special  study  results,  State  microscopic
evaluations, and plant daily records indicate that  the
plant is not effectively removing particles found in  the
raw water. Should a significant  number of  parasitic
organisms such as Giardia cysts or Cryptosporidium
oocysts occur  in  the raw  water (for example,  as a
result  of  cattle  feeding  on  the  grass  above  the
infiltration  system), they would likely enter the  plant
and pass  through the  filter.  Since some  cysts  are
resistant to disinfection  by chlorine,  they could pose a
significant health hazard to the community.

Performance-Limiting Factors
The factors identified as  having a major effect on
performance  on  a long-term  repetitive basis  were
prioritized and are  summarized below:

1.   Water Treatment Understanding - Operations: The
    plant  superintendent/utilities  director  is a  very
    motivated operator;  however, he has not  received
    any formal  training  in  water  treatment practices.
    This  is compounded by   the  complexity of
    operating a direct filtration plant treating cold,  low
    alkalinity,  low turbidity water. Lack  of  water
    treatment understanding was identified  as the  top
    ranking factor because  it has  led to poor operating
    decisions, such as little or no change in chemical
    feed  rates,  filter backwashing based on headloss
    rather  than filtered  water  quality, and  bypass of
    untreated raw water to  the treated water storage
    reservoir. Operation of the  plant  will  require a
    process control program and an understanding of
    coagulation chemistry   including chemical  feed
    calculations.

2.   Process Control Testing - Operations: There was
    no process control  program in place at the plant.
    Operation of  a surface water plant requires that
    testing be  conducted and results  recorded in a
    systematic  manner so  that  data is available to
    make  process control  decisions. Control of  the
    direct filtration plant will  require  daily monitoring of
    influent turbidity,  continuous monitoring  of  filter
    effluent turbidity,  and jar testing  to select
    appropriate coagulant  aids  and  to determine
    optimum chemical doses.

3.   Process Automation -  Design:  The plant is  not
    equipped with  a continuous reading  and recording
    turbidimeter,  which is  necessary  to  adequately
    monitor plant performance since the staffing levels
    do not allow turbidity tests to be conducted  more
    than  once each  day. A continuous  reading
    turbidimeter would allow filter performance to be
    monitored following a backwash so that chemical
    feed could be optimized to reduce the increase in
    turbidity  (turbidity  spike)  that occurs  after a
    backwash.

4.  Disinfection - Design: A detention time of 2 hr is
    needed  to ensure  effective  disinfection  of  the
    treated water  prior to the first  user. The new
    regulations that will be promulgated as a result of
    the SWTR  and/or current  state criteria may
    necessitate capital  improvements before the water
    system has adequate disinfection  capability.  An
    example  of a capital  improvement would be  the
    installation of baffle walls in the clearwell to keep
    the water in the basin  longer for disinfection rather
    than taking a direct route through the basin from
    the influent to the effluent  pipe.  This factor was
    asterisked  because the final  rule will not  be
    effective  until June 29,   1993,  following
    development of State criteria in 1990.

5.  Filtration  -  Design: The filter is  presently being
    operated  at  too high  a rate  to expect adequate
    performance on a continuous basis. In addition,
    warping  of the  filter  section  dividers and   the
    potential  inability  of the  travelling backwash
    mechanism  to  properly wash the filter  could
    impact  filter  performance.   This  factor was
    asterisked because it may  be  possible for  the
    plant to operate at a flow rate consistent with its
    capability, if  water use is  reduced to  normal
    levels. Under this condition, the filter dividers and
    backwash may prove not to significantly impact
    performance.

Factors identified as having either a minimal effect on
a routine basis, or a major effect on  a periodic basis
are summarized below  in order of  priority.

1.  Process Controllability - Design: The effluent flow
    meter does not adequately measure the plant flow
    rate because  it is located  downstream  of   the
    finished water storage reservoir. The flow rate  out
    of  the reservoir is  not indicative of the plant flow
    rate. Since  accurate  flow  measurement is   the
    basis  for  chemical feed calculations  and filter
    hydraulic  loading rates, actual plant flow needs to
    be accurately measured.

2.  Laboratory  Space  and Equipment - Design: The
    plant is  not equipped with a jar test  apparatus.
    Because  of  the raw water  quality characteristics
    (low turbidity, alkalinity, and temperature), special
    studies with various coagulant and flocculant aids
    will  likely  be  required  to  optimize  plant
    performance.  A  jar  test  apparatus  will  be
    necessary to conduct the special studies as well
    as to optimize plant chemical feeds.'

3.  Alarm System  - Design:  There  were no  alarm
    systems  in  the plant  to warn  the operator  of
                                                   71

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    problems,  such as chemical feeder shutdown or
    raw water quality changes. Since the plant is only
    checked once each day  for  about 1  hr,  it is
    essential  that  alarms be  provided  to  warn  the
    operator of a change in conditions.  If alarms are
    not provided, the plant should be staffed any time
    it is in operation.

4.  Watershed  Management - Design: Allowing cattle
    to  graze on top of the infiltration system provides
    an  unnecessary  public health  risk.  Cattle  are
    known carriers of Cryptosporidium, a  parasitic
    cyst that   is extremely  resistant  to  chlorine
    disinfection  and  small  enough to  easily  pass
    through a  poorly operated filter.  A direct filtration
    plant  provides a limited number of barriers to
    pathogenic organisms and limited response time
    for the operator to react to a change in raw water
    quality.

No factors in the administration or maintenance areas
were identified as impacting performance.
Projected Impact of a CCP
Plant 9 produces water that poses a significant health
risk to consumers. Conducting a CCP could result in
an improvement in  finished water quality,  especially
during and after filter backwashing. However, because
peak water demands exceed the rated capacity of the
filter and disinfection system, the plant would have to
be operated at a lower flow  rate. In addition, design
aspects  of the filter  such  as  backwashing
effectiveness and uneven  filter dividers,  could  limit
filter performance to the extent that the plant could not
meet regulatory requirements on a continuous basis.
The CCP might discover that limitations in the filtration
system  require  major capital  improvements to ensure
continuous compliance with applicable regulations.
                                                    72

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 Plant  10

 Facility Description
 Plant 10  is  a conventional water  treatment plant
 supplied from a nearby river that provides water for
 domestic  use. The peak operating flow for the plant
 was established  at  22 Us (0.5  mgd) based  on  a
 review of  flow records for the previous year. The plant
 is normally  operated for approximately  8  hr/day;
 however,  on several  days the plant  is operated for
 longer than 8 hr to meet demands of peak water use.
 On these days,  the treatment processes are  still
 operated only at the 22-L/s (0.5-mgd) flow rate. Plant
 10 consists  of the following unit processes,  shown
 schematically in Figure 4-45:

 •  Intake  structure located on the bank of the river,
   consisting  of a manhole intake structure and a  wet
   well from which raw-water pumps deliver the water
   to the plant. A bar screen is provided between the
   manhole intake structure and the wet well

 •  Three manually operated vertical turbine  raw water
   pumps; two 22 Us (350 gpm) and one 16 Us (250
   gpm)

 •  Raw  water flow measurement consisting of  an  20-
   cm (8-in) orifice meter with  a chart recorder. Also,
   a manual rate-of-flow controller

 •  Volumetric feeder each  for  alum,  lime,  and
   powdered activated carbon

 •  Two  9.1-m (30-ft)  diameter  sedimentation basins,
   each with a surface area of 66 m2 (707 sq ft) and  a
   volume of 307,000 L (81,100 gal)

 •  Two 19,300-L (5,100-gal) recarbonation basins

 •  Four 2.6-m x 3.0-m (8.7-ft x  10-ft) filters with 61  cm
   (24 in) of sand media

 •  94-L/s (1,500-gpm) backwash pump

 •  Gas chlorination system

 •  Two clearwells:  one with  a  capacity of 567,750  L
   (150,000 gal)  and the  second  with a capacity of
   56,775-L(15,000-gal)

 •  Two 47-L/s (750-gpm) vertical turbine high-service
   pumps

 •  Venturi-type  flow  meter,  totalizer,  and   chart
   recorder

Water from the river is pooled behind a low head dam
across the river  downstream of the intake  structure.
Several  pipes extend  out into  the  river  from  the
manhole intake structure allowing  water to be  taken
from different locations. The water then flows  to  the
wet well  where  it is  picked  up  by the raw  water
pumps.

Raw water pumps located on top of the wet well move
the raw water from the intake structure  to the plant.
Only  one  of the  22-L/s  (350-gpm)  pumps is  used.
Though the plant was originally designed for 44 Us
(700 gpm), the plant staff feels that 22 Us (350 gpm)
is the maximum flow that can  be handled because of
limitations  with the sedimentation basins.  Since the
plant  is operated  at a constant rate of  22 Us  (350
gpm), variations in water demand are met by varying
the length of time the plant is operated. Raw water
flows entering the  plant are measured and recorded. A
manual rate-of-flow controller is  available though not
normally used.

Volumetric feeders discharge dry chemicals into tanks
below the feeders, where water is added and mixed to
make  a  slurry.  As the raw  water  flows to  the
sedimentation basins,  alum and  lime  are  added as
slurries into the  pipe.  Chemical  feed rates can be
adjusted by varying the amount of chemical  added to
the slurry tanks. These adjustments  are  made based
on observations  of floe  formation in  raw water
samples that have been placed on a magnetic stirring
apparatus after chemical feed. No mechanical or static
flash mixing is provided.  Chemical feed rates are not
routinely adjusted.

After  chemical  addition,  raw water flows to the two
sedimentation  basins.  These  units were  originally
designed as a type of upflow  solids contact clarifier,
eliminating the  need  for separate flash  mix  and
flocculation processes,  but  they  are  no longer
operated as designed.  Flow enters through  a 20-cm
(8-in)  pipe at the bottom of the  unit and strikes a small
baffle redirecting the flow in the  basin. Basin effluent
discharges through peripherally mounted submerged
orifice weirs.  Each basin originally had  a  rotating arm
located near the bottom powered by pressurized basin
effluent.  Basin  effluent was to  be withdrawn  and
pumped back through nozzles in the arm  causing it to
rotate and promote flocculation. The  rotating arm has
been  removed  from one of the  units  and is  not
operational  in  the  second.  Sludge is  manually
removed from the basins twice  a  year. The  plant
discharges this  sludge  to  the sanitary sewer or back
to the river.

Settled water flows by gravity from the sedimentation
basins to the four sand filters and is controlled by float
valves in the recarbonation basins. These valves  shut
off sedimentation  basin effluent flow if the level in the
filters  exceeds  the  maximum.   Operators  visually
monitor the filter water levels and adjust the flow using
rate-of-flow controllers.  Flow meters  are  available for
each filter, but are  not used for  filter flow adjustment.

During  the CPE, the  standard  practice  for  filter
backwashing was to wash two  of the filters each day
                                                  73

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Figure 4-45.  Plant 10 process flow diagram.
                                                          74

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using backwash water from Clearwell 2. Headless or
turbidity  measurements  were not  typically used to
initiate backwashing. The backwash pump discharges
through  a rate-of-flow controller,  but there are  no
valves that can easily be operated to  slowly start and
stop the backwash flow to the filters. The  surface of
the sand is manually raked during the backwashing.
The plant discharges backwash  water to the sanitary
sewer or to the river. During the CPE, the backwash
water was being discharged to the river.

Water from all four filters is discharged to Clearwell 1,
immediately following injection of chlorine gas into the
pipe.  Chlorine  doses  are controlled to  provide  a
residual of 2.5-3.0  mg/L Finished water normally flows
from Clearwell  1 to Clearwell 2; piping is provided to
allow bypassing of Clearwell 1.  Clearwell 2 also
serves as the  suction pipe for  the high-service  and
backwash pumps.

Two high-service pumps supply finished water  to the
two in-ground storage tanks that feed the village water
distribution  system.  These  pumps  are  operated
manually based on  water  levels in  the storage
reservoirs.

Major Unit Process Evaluation
The performance potential graph is shown in Figure 4-
46. Flocculation is  a key major unit treatment process.
As originally designed,  the sedimentation basins were
to  provide  both  flocculation and  sedimentation;
however, the flocculation aspect of these units  has
been removed or is inoperable. The CPE team doubts
that the  units were  ever  capable of  providing
acceptable flocculation even if operated as designed.
As  such, the flocculation process was given a peak
instantaneous  rated capacity  of  0 L/d.  This  rating
implies  that  the   plant  cannot   be expected  to
consistently produce the  desired water quality of less
than 0.5  NTU  without adding flocculation process
capabilities.

The sedimentation  basins were rated  at 12 L/s (0.28
mgd) based on  a surface overflow rate of 8.1 m3/m2/d
(200  gpd/sq  ft).   The  surface  overflow  rate  is
significantly  lower than that for other types  of circular
sedimentation basins with the same  depth as Plant
10. The  projected  peak  instantaneous  operating
capacity  of  the sedimentation basins was lowered
because of  the extremely poor inlet conditions. With
the inlet structure  located  in  the  bottom of  the
sedimentation  basins,  the influent  flow disrupts  the
settled  solids  and  tends to carry  them  upwards
towards the effluent. Properly designed sedimentation
basins introduce the influent water near the surface
through an inlet structure that directs the flow into the
basin,  promoting the separation  of solids from  the
clarified liquid over  the entire surface area. This  allows
the separated solids to move  by gravity to the bottom
of the basin and the clarified effluent  to move  to the
sgrface where it is  removed.
The filters were rated at 22 Us (0.50 mgd) based on a
filter loading rate of 58  m3/m2/d (1 gpm/sq ft). This
loading rate  is lower than typical values because of
the air binding observed  by the CPE team during filter
backwashing. Air binding results  in air pockets in the
filter media,  which  prevents water  from  passing
through that portion of the  filter, effectively lowering
the  surface  area available for  filtration.  The filter
loading  rate,  therefore,  was  lowered  in  the
assessment to compensate for the loss of filter area
due to the observed air binding.

The disinfection  system  was rated at 24  L/s (0.54
mgd). Future drinking water regulations for disinfection
will be based on CT values found to  be needed  for
various removals of Giardia cysts and inactivation of
viruses. CT is the disinfectant concentration multiplied
by the actual time the finished water is in contact with
the disinfectant. To establish the CT required,  it was
assumed that the  plant's disinfection  system  would
have to provide 2 logs (99 percent) of cyst removal
with 2 logs of removal credited for the other treatment
processes.  The total  of 4  logs  of  cyst  removal
required for the plant was based on the CPE team's
estimate of the quality of the raw water.

To  achieve the 2 logs of cyst  removal, the CPE team
estimated that the disinfection system  would have to
provide a CT of 133. This CT value  is for chlorine at a
2.0 mg/L dose, pH 7.5,  and temperature of  5C. The
contact time was based  on  the chlorine  being  added
ahead  of Clearwell 1  and the flow passing through
both clean/veils. Only  15 percent  of the  theoretical
detention time in the clearwells was used because the
clearwells are  not baffled  and  because they  are
subjected to fill and draw operation.  The actual levels
of disinfection required for the plant in the future will
be determined by the State. The CPE estimates of the
required  total  number of  log  reductions  and  the
allowances for actual contact  times in the clearwells
may change when  the  final  state regulations  are
developed.

The performance potential graph  shows that  the lack
of flocculation severely limits  the capabilities of  the
treatment  processes. Without adequate flocculation,
the CPE team  estimates that there is essentially  no
flow where the required performance can be obtained.
The sedimentation basins  also  severely  limit  the
capacity  of  the  plant, even  if adequate  flocculation
was provided. These processes prevent the plant from
achieving  desired  performance at  the  current peak
instantaneous operating flow rate of  22 L/s (350 gpm).
The filters and  disinfection system  were projected to
be adequate to treat this flow.

Performance Assessment
Turbidity data from the plant records  for the raw
water,  settled water from the sedimentation basins,
and  finished  water  over  a 1-yr period  are plotted in
Figures 4-47, 4-48, and 4-49, respectively.
                                                   75

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Figure 4-46. Plant 10 performance potential graph,


    Unit Process
                                           0.1
                                                      0.2
                     Flow, mgd ,

                        0.3
                                                                              0.4
                                                                                          0.5
                                                                                                     0.6
    Sedimentation1
      SOR. gpd/sq ft


    Filtration2
      HLR, gpm/sq ft


    Disinfection?
      Contact time, min
70
            141
0.2
            0.4
                        0.6
                                   0.8
356
            178
                        119
                                    89
                                               71
                                                                                 Peak Instantaneous Operating
                                                                                  Flow (1 Pump) = 350 gpm


   1 Rated at 200 gpd/sq ft because of poor inlet conditions, turbulence at the basin bottom, and poor durface area development.
   2 Rated at 1 gpm/sq ft because of observed air binding.
   3 Rated at CT - 133 with 2 mg/L chlorine dose, which requires a 67-min HOT; allowed 15 percent of available volume dfor contact
    time, temperature s 5ฐC, pH = 7.5, 4-log required reduction, 2 allowed for plant.
Figure  4-47  shows  the fluctuation  of raw water
turbidity over the year.  Well-designed and  operated
treatment processes are  expected to produce a water
with  consistent turbidity levels  even with  wide
variations in raw water turbidity. As shown in  Figure 4-
48, the sedimentation  basins produced a settled water
that also had significant variations  in turbidity. The
filters  reduced  the  levels  of  turbidity, as  shown in
Rgure  4-49,  but still  experience variations  as  raw
water turbidity changes. These results indicate design
and/or  operational  problems.  Figure 4-50 shows the
finished water turbidity during  a 6-month period when
the  plant was treating a highly variable turbidity  raw
water.  The   applicable  regulation  for  turbidity is
currently 1.0  NTU.  Future  regulations  will require the
plant to meet a 0.5-NTU finished  water turbidity 95
percent of the time. Figure 4-50 shows that  the  plant
generally complies with the 1.0-NTU regulation, but is
consistently above the 0.5 NTU required by the future
regulations. A  probability plot of this same data is
shown  in Figure 4-51,  which  indicates that under
present conditions the plant would only meet the  0.5-
NTU standard approximately 50 percent of the time.

During the CPE, a special study was completed to
assess the filter performance  after backwashing. With
adequate  facilities  and  operation of  preceding  unit
processes, a  properly operated filter should produce a
finished water turbidity of approximately 0.1  NTU and
only experience a 0.2-NTU  rise in  turbidity in the
finished water  for  approximately  10  minutes  after
restart following backwashing.  Filters 3  and 4  were
sampled for a 30-minute period after  restart following
backwashing. The  results of this  special  study are
shown  in Figures  4-52  and 4-53.  Both filters
             experienced an approximately 0.3-NTU rise in turbidity
             that did not drop back to the original value even after
             30  minutes.  These  results could indicate  a problem
             with the filters or that the water being applied to  the
             filter has not been properly treated and conditioned in
             the preceding unit processes.

             An  evaluation of the filter media was also performed
             during the CPE.  The evaluation team determined that
             the filters  were being adequately backwashed,  since
             no  significant  mudballs  were found.  They  did  find
             some  buildup  of chemicals  on the  surface of  the
             media, but  these  were not considered  to affect
             performance. Air binding was also observed during  the
             special studies.

             Performance-Limiting Factors
             The factors  identified  as having a major  effect on
             performance  on  a  long-term repetitive basis  were
             prioritized and are summarized below:

             1.  Flash  Mix and  Flocculation  -  Design: The plant
                 has no  flash  mix  or  flocculation  treatment
                 processes, facilities which are required  to properly
                 condition the raw water with chemicals prior to the
                 sedimentation and filtration treatment  processes.
                 Without  these  capabilities  the plant  will  have
                 significant problems  removing enough  turbidity to
                 consistently meet future regulations.

             2.  Sedimentation  Basins -  Design:  Adequate
                 sedimentation basins are required to remove  the
                 coagulated  turbidity from  the  raw water.  The
                 sedimentation basins have basic limitations related
                 to the lack of a proper inlet structure. At current
                                                     76

-------
Figure 4-47.  Raw water turbidity profile - Plant 10.
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           RUG88      OCT       DEC     FEB89     RPR       JUN      RUG      OCT
Figure 4-48. Settled water turbidity profile - Plant 10.
           RUG88     OCT       DEC      FEB89     RPR      JUN       RUG
OCT
                                              77

-------
Figure 4-49.  Finished water turbidity profile - Plant 10.
           in
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Figure 4-51.  Probability plot of finished water turbidity - Plant 10.

           en
              . 1
    10                 50
         Probability
99       99.9
Figure 4-52.  Fiulter 3 effluent turbidity profile after backwash
             - Plant 10.


 Turbidity, NTU

   0.8  r-
   0.6
   0.4
   0.2
                       I
J
                      10      15     20

                            Minutes
        25     30
                           Figure 4-53.  Filter 4 effluent turbidity profile after backwash •
                                        Plant 10.
                            Turbidity, NTU

                              0.8   r-
                                                                   0.6
                                                                   0.4
                                                                   0.2
                                                         I
                                                                                                      I
                                                 10
                                                         15     20

                                                       Minutes
              25      30
                                                            79

-------
    loadings  (e.g.,  22 L/s  [350 gpm]),  the basin
    limitations allow high turbidity water to pass to the
    filters, thus degrading their performance.

3.  Number of Plant Staff - Administration: Currently a
    staff  of three persons have  responsibility for the
    operation and  maintenance  of  the  water plant,
    wastewater  plant,  distribution  system, and
    collection system. CPE interviews with the Board
    of Public Affairs revealed that a fourth person may
    be hired after construction of the new wastewater
    treatment plant is completed. To  respond to the
    variations in  raw  water turbidity,  increased
    coverage of the water  plant to  make  process
    changes will be needed. Given this requirement
    plus  other observed responsibilities,  even a staff
    of four may be inadequate.

4.  Application of  Concepts and Testing to  Process
    Control - Operation: The plant staff appeared to
    have  proper  training,  understood 'the basic
    concepts of  process  control,  and  were  very
    motivated. However, the chemical doses were not
    changed based  on  changes  in  raw  water
    characteristics,  the alum dose  measured  during
    the  CPE was  excessively high,  and  the filters
    were operated without adequate  consideration of
    the  turbidity   levels  in  the  filter effluent.
    Additionally,  dirty filters were regularly  started
    without any  assessment of  the impact  of this
    practice on filter effluent turbidity levels. Because
    of these practices, the CPE  team assessed that
    the  planf staff  was  not  consistently applying
    proper water treatment concepts and  process
    control  testing  to  optimize the  plant's
    performance.

Factors identified as having either a  minimal effect on
a routine basis or  a major effect on a periodic basis
are summarized below in order of priority.

1.  Filtration  - Design:  The  configuration  of  the
    filtration system allows conditions that create  air
    binding in the filters. The air  binding is caused by
    negative  pressures  being  created  in the filter
    media  as solids are  removed  and headloss
    increases. This causes  the  dissolved air  in the
    water to come out of solution and be retained in
    the filter  media.  Water cannot pass through the
    portions of the media where the  air  is retained,
    which  effectively  reduces   the surface  area
    available for  filtration. This condition reduces the
    plant's capacity and  can significantly affect filter
    performance.
2.  Lack  of  Preventive  Maintenance  Program -
    Maintenance:  The  plant  has  no  formalized
    preventive maintenance program. Equipment  is
    repaired as it breaks down. A lack of maintenance
    of  a number of key  pieces  of  equipment was
    considered  to  have a minimal,  but continuous
    impact on  performance.  This key equipment
    included the alum feeder, filter flow measurement
    devices and control valves,  chlorinator controls,
    clarifier equipment  including  the weirs, and the
    raw water pumps. Plant staffing levels appeared to
    impact the level  of preventive maintenance, but
    even with adequate  staff  a  formalized program
    would be  needed  to  assure  availability  of  key
    equipment.

3.  Chemical  Feed  Facilities  -  Design: The  plant
    needs  additional  chemical  feed  facilities  to
    consistently  meet required  performance.  A
    polymer  feed  system  is  projected   as  a
    requirement  to  optimize  filter  performance,
    especially during  cold weather operation.  A
    backup alum  feeder would also be required to
    assure a consistent source of chemical feed.

4.  Alarm Systems -  Design: The plant is operated for
    significant  periods of time without any operations
    staff present  to  make process  adjustments in
    response to variations  in raw water characteristics
    or   correct  problems with  key  processes
    equipment.   During  periods  of  unattended
    operation  process performance could degrade to
    a point where  it  poses a potential health  risk to
    the  village. A turbidity monitoring  system  tied to
    raw and finished  water could  be used to alert the
    plant staff to process  problems before  finished
    water quality reached undesirable levels.

The age of some of the equipment was identified as a
minor factor  limiting  performance.  Though   not  a
performance-limiting  factor, the current  practice of
disposing of sludge and backwash water into the river
is in violation of State regulations.

Projected Impact of a CCP
The CPE identified numerous design problems related
to the key unit treatment  processes, which must be
corrected before  any  process optimization through
use of a CCP could be successful. A CCP, therefore,
was not recommended.
                                                  80

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Plant 11

Facility Description
Plant 11  is a conventional  water treatment plant that
treats water from a nearby river for domestic  use  by
the village. Based on a review of flow records for the
previous  year, the peak  operating flow for the plant
was established  at  19  Us  (0.43 mgd). Plant  11
consists  of the  following  unit  processes  shown
schematically in Figure 4-54.

•  Intake  structure

•  49 million-L (13 mil-gal) reservoir

•  Three  vertical turbine raw water  pumps: two 19 Us
   (300 gpm) and one 38  L/s (600 gpm)

•  19-L/s (300-gpm) submersible raw water pump

•  Metering pump to feed a ferric chloride solution

•  Two volumetric  feeders, one for lime and another
   for alum addition

•  Rapid  mix basin with a surface area of 0.46 m2 (5.0
   sq ft);  and a depth of 0.6 m (2 ft)

•  Solids contact clarifier  9.1 m (30 ft) in diameter and
   3.8-4.1 m (12.5-13.6 ft) deep; flocculator  volume,
   29,800 L (7,875 gal); clarifier effective surface area,
   61.6 m2 (663 sq ft), and volume, 205,330 L (54,250
   gal)

•  Three  dual media filters, two 2.4 m x 2.5 m (8 ft x 8
   ft), and one 2.1  m x 2.7 m (7 ft x 9 ft) that contain
   46-51  cm (18-20 in) of sand and 20-25 cm (8-  10
   in) of anthracite media

•  Vacuum-controlled solution  feed  chlorination
   system fed from 68 kg (150-lb) cylinders
   151,400-L (40,000-gal) clean/veil

   321,725-L (85,000-gal) clearwell
   Two 24-L/s (375 gpm) vertical turbine high-service
   pumps

   15-cm (6-in) orifice  plate with a totalizer-indicator-
   recorder
Water from the river  is pooled  behind a  low dam
across the river downstream of the intake structure.
River water is normally pumped to the reservoir by the
submersible pump. Water from the  reservoir flows by
gravity to the  wet well beneath the intake structure,
where it is pumped to the plant by the vertical turbine
raw water pumps. These pumps can  also pump river
water directly to the plant, bypassing the reservoir.
Raw water flows to the rapid mix basin  where ferric
chloride solution  is added via a diaphragm metering
pump. A hydrated lime slurry is also fed into the rapid
mix basin  via a volumetric feeder. A volumetric feeder
is in place to feed alum, although it is currently not is
use. Flash mixing was not performed during the CPE
due to a bearing problem with the mixer. However, the
CPE team calculated the G value for the rapid  mix
basin to be adequate at 1,418 sec-1 if the mixer were
operating. Chemical feed  rates  can  be  adjusted
manually  by  the amount  of chemical  added  to  the
slurry tanks,  or by  adjusting  the stroke  on  the
metering pump, but they were not routinely changed.

Raw water flows to the center flocculation cone of the
solids contact clarifier. After flocculation,  water enters
the outer  clarifier portion of the unit and is removed
through  peripheral v-notched weir  troughs. Sludge is
periodically removed  automatically from  the  clarifier,
through  use of a timed blow-down, and discharged to
a  sanitary sewer for disposal at the wastewater
treatment  plant.

Settled  water  flows by  gravity  from  the  reactor
clarifiers  to  a  basin  (originally designed as a
recarbonation  basin),  where the flow is split to  the
three filters.  Rate  of  flow through  the filters is
controlled  by float-activated  butterfly valves that open
or close to maintain a constant water level above the
filter media.

Filter runs are  normally  24-27  hr, with  the plant
operating  a  total of  8-9  hr/day.  One  filter is
backwashed each day, so that filters operate  3 days
before  backwashing.  No individual filter  headloss or
turbidity monitoring equipment exists,  although  the
village intends to install headloss  gauges.  Backwash
water is supplied by distribution system pressure from
operation  of the  high-service pumps.  The backwash
rate was determined  during  the   CPE  to  be
approximately  1,110  m3/m2/d (19  gpm/sq ft).  The
surface  of  the  media is  manually  raked  during
backwashing.  Backwash  water is  discharged  to  the
sanitary sewer.

Water from  each filter flows through  separate pipes
into  Clearwell  1, where a chlorine  solution  is injected
to maintain  residuals  between  2.3 and 2.5 mg/L.
Finished water  normally flows from Clearwell 1  to
Clearwell 2. The high-service pumps take suction from
Clearwell 1.

Two high-service pumps supply  finished  water to the
two  elevated storage  tanks that feed the water
distribution  system.  These pumps  are  operated
automatically based  on water levels in the elevated
storage  tanks. The plant comes on and  off line usually
two  to three times during the day based on water
levels in the clearwell. Typically,  the plant operates 8-
9  hr/day  at a  constant  rate of 24 Us (375 gpm).
                                                   81

-------
Figure 4-54.  Plant 11 process flow diagram.
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Variations in demand are met by varying the length of
time the plant is operated.

Major Unit Process Evaluation
The performance potential graph is shown in Figure 4-
55. The instantaneous peak operating flow of 19 Us
(0.43 mgd) assumes that only one of the small raw
water pumps will supply the plant.

The flocculation capabilities  of the reactor clarifier
were rated at 25 L/s (0.57 mgd) based on achieving a
hydraulic  detention time of 20 minutes.  This rating
depends on  retrofitting the  basin  with the variable
speed drive  for the mixers, which was included in the
plant's original design.

The sedimentation  capabilities  of the reactor  clarifier
were rated at  22 L/s (0.50 mgd) based on a  surface
overflow rate  of  30  m3/m2/d  (750 gpd/sq ft). The
projected  capacity of the basins was lowered due to
the constraints of the 3.8- m (12.6-ft) basin depth.

The filters were rated at 36 L/s (0.82 mgd) based on a
filter loading rate of 176 m3/m2/d  (3 gpm/sq ft). This
loading  rate was decreased from more typical values
for dual media  filters because of  the rate  control
system.

The disinfection system  was rated at  15  L/s  (0.34
mgd). Future drinking water regulations for disinfection
will  be based  on CT values found to be  needed  for
removal of Giardia cysts and inactivation of viruses.
This evaluation  used a  CT of 127, which  is  for
chlorine at a 2.4 mg/L dose,  pH 8.0, and temperature
of 5ฐC. It was assumed that the disinfection  system
would have  to provide 1.5 logs of cyst removal with
2.5  logs of  removal credited  for the other.treatment
processes. The  4 logs of total cyst removal required
for the plant was based  on the CPE team's estimate
of  the potential for contamination  of the raw water.
The contact time  was based  on the  chlorine  being
added ahead  of Clearwell  1  and the flow  passing
through  both  clearwells.  Only  10 percent  of the
nominal  detention  time  in the clearwells  was  used
because  (1) the clearwells  are  not baffled,  (2) the
piping arrangement does not assure that all of the flow
passes through both clearwells, and (3) the clearwells
are subject to fill and draw operation. In the future, the
actual levels of disinfection required for the plant  will
be  determined by the State.  The  estimates of the
required  total number  of  log reductions and the
allowances  for actual  contact times in the  clearwells
may change  after  the  final State regulations are
developed.

As  shown  in the  performance  potential graph, the
major unit  processes,  with the  exception  of the
disinfection  process, have a rated capacity close to or
exceeding the instantaneous peak operating flow. The
flocculation  and  sedimentation  process,  although
borderline,  were  projected  adequate to  treat the
operating flow rate of 19 L/s (0.43 mgd).  The filtration
system,  rated at  36  L/s  (0.82 mgd),  was  rated
considerably  more  than adequate to treat this  flow.
Lack  of  baffling  in the clearwells  and  the piping
arrangement  between  the  two clean/veils limited the
projected capacity of the disinfection process.

Performance Assessment
Figure 4-56   shows  turbidity  data from  the  plant
records. The current applicable regulation for turbidity
is  1.0  NTU.  The plant  normally produces water with
turbidities less than 1.0 NTU,  but is frequently above
the 0.5  NTU level, which will be  required by the
SWTR, as shown in Figure 4-56. A probability plot of
this same  data, shown in  Figure 4-57,  indicates that
the plant  would only meet the  0.5-NTU requirement
approximately 30 percent of the time.

During the CPE, a special study was  conducted to
assess filter  performance  after  backwashing.  With
adequate  facilities  and operation of preceding unit
processes,   a  properly  operated  filter should
experience a 0.2-NTU rise in  turbidity in the finished
water  for approximately  10   minutes  after restart
following backwashing.  Figure  4-58  shows the results
of a study that sampled Filter 3 for a 40-minute period
after   restart following backwashing.  The   filter
experienced  an  approximate 1.0-NTU rise in turbidity
that did not drop back to the original value even after
40 minutes. This delay may be attributed to a problem
in the  filter, or to improper  treatment and conditioning
of the  water prior to filtering.

After backwash, Filter 3 was drained and 2.5- to 3.8-
cm (1- to  1.5-in)  mudballs were  observed in the
media. As mudballs increase in size, they can settle to
the bottom of the  media  and limit  the  flow through
these  portions of  the  filter.  The filter  flow is then
forced through the remaining  media at  higher rates,
which  can  impact  filter capacity and  performance.
Proper backwashing  procedures, such  as  adequate
length of  backwash, gradual   increase  in backwash
flow rates, and  sufficient agitation of the media, can
minimize the occurrence of mudballs.

Performance-Limiting Factors
The factors  identified  as  having a major  effect  on
performance  on  a  long-term  repetitive basis  were
prioritized and are summarized below:

1.  Application  of  Concepts   and  Testing  Process
    Control - Operation: Several operational practices
    performed by  the  plant staff,  including  applying
    ferric  chloride  and lime at the  same  point,
    regularly started dirty filters, and an  unawareness
    of the condition of  the  filter media, impaired plant
    performance. Lime  raises  the raw water pH above
    the  range   necessary  to  achieve  optimum
    coagulation  and flocculation  using ferric chloride.
    Starting  dirty filters without monitoring the impact
    on finished  water turbidity  may  represent  a
                                                  0-83

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Figure 4-55.  Plant 11 performance potential graph.
     Unit Process
                                                0.2
                                                             0.4
                                       Flow, mgd


                                         0.6
                                                                                       0.8
                                                                                                    1.0
     Flocculatlon1

       HOT, min



     Sedimentation2

       SOR, gpd/sq ft



     Filtration*

       HLR, gpm/sq ft



     Disinfection4

       Contact time, min
               57
                            28
               302
                            603
               0.7
                            1.5
                                                90
                                         2.2
                                                      2.9
                                                       Peak Instantaneous Operating
                                                        Flow (1 Pump) = 350 gpm


   1 Rated at 20 -min HOT - assumes variable speed drive would be added.
   2 Rated at 750 gpd/sq ft - 12.5-ft depth discourages higher rating.
   3 Rated at 3 gpm/sq ft. Rate control system considered limiting.
   * Rated at CT - 127 with 2.4 mg/L chlorine dose, which requires a 53-min HOT; allowed 10 percent of available volume for contact
    time, temperature  = 5ฐC, pH = 8, 4-log required  reduction, 2.5 log in plant, 1.5 log disinfection.
Figure 4-56.  Raw water turbidity profile - Plant 11.



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                                                                                                           Present
                                                                                                         Requirement
                                                    Future
                                                  Requirement
MRR88
                      MRY
JUL
                             SEP
NOV
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MRR
MRY
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                                                          84

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Figure 4-57.  Probability plot of finished water turbidity - Plant 10.

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    The State's interpretation of this rule may lead to
    different  results  than  indicated  by  this
    evaluation.Factors identified  as having  either  a
    minimal effect on a routine basis or a major effect
    on a periodic basis are summarized below in order
    of priority.

1.  Supervision - Administration: There is  no clear
    definition or delegation of responsibilities between
    the superintendent and  other members of  the
    staff.  To maintain continuity in plant operations,
    specific tasks should be assigned  to each staff
    member. This  would alleviate incidents of  poor
    communication between the plant  staff (e.g., staff
    members arbitrarily resetting chemical feed rates
    after  they  have  been  adjusted  by  other  staff
    members).  Once plant  personnel  have  clear
    definition of  duties, daily  planning  and priority
    setting, which  is  presently minimal,  can be
    optimized to increase plant performance.

2.  Process Accessibility for Sampling - Design: The
    lack of sampling  locations to evaluate various
    plant  unit  processes limits implementation  of an
    acceptable process control program. At minimum,
    the plant should  have  taps to determine influent
    and effluent turbidity levels for the reservoir (and
    river,  if pumping  directly  to the  plant),  solids
    contact clarifier, each of the three filters,  and both
    clean/veils.

3.  Alarm Systems - Design: The plant is operated for
    significant periods of time without any operations
    staff  present  to  make process  adjustments  in
    response to variations in  raw  water characteristics
    or  correct  problems  with  key  processes
    equipment. As such, finished water quality  could
    degrade and pose  a potential health  risk  to  the
    village. A turbidity monitoring system  tied  to  the
    clean/veil effluent  could be  used to alert the plant
    staff to process  problems before finished  water
    quality reaches undesirable levels.

4.  Number of Plant Staff - Administration: Presently,
    a staff of four persons have  responsibility for the
    operation and  maintenance  of the  water  plant,
    wastewater  plant, distribution system, collection
    system, and  street maintenance.  To  properly
    respond to the variations in  raw  water  turbidity,
    implement  a process  control  program, provide
    sample taps, etc., increased coverage of the plant
    will  be needed. Given these  responsibilities and
    requirements, a staff of four is inadequate.
5.  Plant  Staff  Morale  Pay  - Administration:  The
    current pay structure for the staff may discourage
    more  highly  qualified  people from  applying  for
    operator positions. The village does not currently
    offer a pay scale competitive with other facilities.

6.  Chemical Feed Facilities -  Design: The plant lacks
    the capability to feed  chemicals to  various points
    in  the treatment process. The option to apply
    chemicals (e.g., lime)  will  enable optimal use of
    chemicals  and chemical  dosages.  Additional
    chemical feed facilities were  projected  to  be
    required. A polymer feed system could be used to
    optimize filter  performance especially during  cold
    weather operation.

The CPE  team identified additional  factors that had  a
minor  effect  on plant performance. Specifically,  the
lack of a preventive maintenance program, the lack of
variable speed mixing capabilities during  flocculation,
and  the minimal  depth of the sedimentation  basin.
Headloss  gauges should also  be installed on each of
the filters to enable optimization of filter runs based on
headloss and/or effluent turbidity levels. The  inability
to control  flow distribution  to the filters and control  the
rate of  flow at each  filter will  also  adversely impact
filter operation.

Projected Impact of a CCP
Alleviating the  identified  factors would  appreciably
improve the  performance of  Plant  11. As such,
implementation of a CCP, if accepted  by the village
personnel, represented a viable option for the plant.
                                                   86

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Plant 12
   Propeller-type finished water flow meter
Facility Description
Plant 12 is a conventional plant that treats water from
a nearby river to provide water for domestic  use by
the city.  It consists of two separate sets of treatment
process  trains that operate in parallel. One of these,
designated the  "old"  plant,  consists  of the solids
contact clarifier and the two circular dual media filters.
These were  the original  treatment processes before
the plant was  expanded  in  1977. The  second  set,
designated the  "new" plant, consists  of two package
plants. Based on a review of plant records, the  peak
operating flow for the  entire  plant was 32 Us (0.72
mgd). Plant 12 consists of two separate sets of unit
processes shown schematically in Figure 4-59.

• Raw  water   intake  structure containing   two
  submersible pumps:  one 25 Us (400 gpm)  and the
  other 31 L/s (500 gpm)

• Propeller-type raw water flow meter

• Seven  volumetric chemical feeders: two for alum,
  three  for  lime,  one  for  fluoride,  and  one for
  KMnO4/PAC

• Two 3.4-m (11-ft) diameter flocculation basins, 2.7
  m (8.8 ft) deep, each equipped with vertical paddle
  flocculators and variable speed drives. Each unit is
  divided into two sections by a mid-depth horizontal
  perforated  baffle

• Two package plants each  with sedimentation  and
  filtration. The  sedimentation section has a surface
  area of 4.8 m2 (51.8 sq ft) and contains a 1.7-m
  (5.7- ft) high  module  of 7.5-degree tube settlers.
  Each filter  has 10.2  m2 (110 sq ft)  of surface  area
  and 76 cm (30 in) of mixed  media

• 6.4-m  (21-ft)  diameter, 3.0-m  (10-ft) deep  upflow
  solids  contact clarifier.  Center flocculation cone has
  a volume  of  8,515  L (2,250 gal)  with  a  vertical
  paddle mixer

• Two  2.7-m  (9-ft)  diameter  dual  media  filters
  containing  69 cm (27 in) of  media

• Two clearwells: one  "old",  with 246,782-L (65,200-
  gal) capacity and the other "new",  with 199,470-L
  (52,700-gal) capacity

• Two backwash pumps: one  "new"  63 Us  (1,000
  gpm),  and  the other "old", est. at 31 L/s (500 gpm)

• Vacuum-controlled  solution  feed  chlorination
  system fed from 68-kg  (150-lb) cylinders

• Three high-service pumps:  two "old", estimated at
  16 L/s (250 gpm) and 38  L/s  (600 gpm) and the
  third "new" 31 L/s (500 gpm)
•  333,080-L (88,000-gal) backwash water and sludge
   holding basin

Water is taken from the middle of the river through an
intake pipe. Either of two submersible pumps is used
to supply raw water to the plant. The plant is operated
usually 6-8  hr/day and  meets higher demands  by
operating for longer periods.

The raw water is split between the "old" and "new"
plant by separate valves at the flow split. Capabilities
exist to pre-chlorinate the raw water.  The raw water
flow meter for the "old"  plant had been removed  for
repair and  had never been replaced.  For the "new"
plant,  raw  water flows can be  measured and
controlled.   During  the  CPE,  the flow meter was
operational, but had  not been  calibrated and,  thus,
was  not used by  the  plant  staff. The rate-of-flow
controller was out of service. Neither the flow meter or
controller had been used for a long time.

Alum and lime are added to  both of the plants using
volumetric  dry chemical feeders. On the "new" plant,
alum and lime slurries were prepared by adding water
to the  dry chemicals in mixing tanks  beneath the
feeders. These slurries  were conveyed by gravity to
the pipe carrying the raw water to the flocculators.  No
mechanical  or  static flash  mixing  was  provided.
Chemical feed rates for both plants were adjusted with
changes in raw water  turbidity based on the operator's
experience. A jar testing apparatus was available at
the plant, but not used.  Feed rates were not routinely
adjusted.

The two flocculators  on the  "new" plant  had  been
modified by  removing  the  horizontal,  perforated
baffles. These  baffles, intended to  separate each of
these  units into  two stages, would  have  provided
improved flocculation. The  mechanical  mixers  on
these basins were also not operational.

From the flocculation  basins,  flow to the "new"  plant
enters a tank that has a sedimentation and filtration
section.  Flow  is  directed  to  the  bottom  of  the
sedimentation section and then flows up through a
module of  7.5 degree-tube  settlers.  Settled  water
discharges  into a trough that conveys it to the filtration
section. After passing through the  mixed media  filter,
the finished water flows to the clearwells.

The filtration units  were designed   for automatic
operation with electrically actuated  valves controlling
the filter flow  rate based on  level measurements.
Backwashing was also  designed  to  use automatic
electrically  actuated valves. Continuous turbidimeters
for the raw and finished  water were provided.  During
the CPE, however, none of the automatic valves or
turbidimeters were  operational.  Instead,  the  plants
were  operated manually,  but the plant  staff could not
                                                  87

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Figure 4-59.  Plant 12 process flow diagram.
                                                         88

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adequately control the flow through the filters. Settled
water was observed cascading onto the surface of the
filter media. When a filter is  properly operated, the
surface of the  filter  media is  flooded, but under the
observed conditions, flow was passing through only a
portion  of  the  media.  Both the filters and the tube
settlers were  backwashed at the  same time using
water pumped  from the clearwells. Backwash water
was discharged to the holding basin.

In the "old" plant, a volumetric feeder adds dry alum
directly into the center  flocculation zone and lime is
prepared  as a slurry  and piped  to  the flocculation
zone.  A mechanical mixer provides  mixing  in the
zone.

The upflow solids contact  clarifier on the "old" plant
consists  of two  sections that  provide  for both
flocculation and sedimentation. Flocculation occurs in
a mechanically mixed  cone-shaped  center section,
while sedimentation  occurs in the outer  portion. Raw
water enters the flocculation  section and then flows
downward before proceeding  through the bottom  of
this section into the upflow sedimentation section. The
mechanical mixer promotes  flocculation  and  settled
water discharges over  peripheral weirs.  Proper
operation of solids  contact  clarifiers relies  on  the
measurement and control  of the solids maintained in
the unit. At the plant, solids levels and concentrations
were not measured or controlled.

The  "old" plant  filters  were  circular steel tanks that
showed significant signs of  corrosion.  Two  troughs
above the media distributed  the settled  water to  the
filters and collected the backwash water.  Filter flow
rates  were controlled  by  float-actuated  valves that
were  intended to  maintain  a constant  water level
above the filter.  During the CPE,  these  valves were
not operational. Settled  water was observed cascading
onto  the  media  surface instead of flooding the filter
media. These  filters  are backwashed with  water
pumped from the clearwells. Backwash  water is then
discharged to the holding basin.

Finished  water from both  plants combines ahead of
the "new" clearwell where chlorine, fluoride, and lime
are added. Chlorine doses are adjusted  to maintain a
residual of 2.0 mg/L in the finished water leaving the
clearwell.  Both pre- and  post-chlorination  are used.
The  staff attempts to  maintain a 50/50  split between
the two addition points, but no provisions are available
to measure this split.

All finished water enters the "new" clearwell,  but both
clearwells  are interconnected  so  that  the flow  is
 distributed  between them.  Separate  high-  service
 pumps draw from each clearwell, an arrangement that
 prevents the  two clearwells  from operating in series,
 and  thereby  optimizing the  contact time  with  the
 chlorine. During  the  CPE,  one  of  the "old" high-
 service pumps had been  removed for service. High-
service  pumps are operated manually to supply the
four storage tanks in the distribution system.

Major Unit Process Evaluation
The performance potential graph is shown in Figure 4-
60. Three sets  of bars are  presented  for each unit
process representing the "old" plant, the "new" plant,
and the  total  for both plants combined.  Disinfection
was only evaluated for the combined plants  because
the units are  interconnected.  The  shortest bar
represents the  treatment process that  limits  plant
capacity to  achieve the desired performance of less
than 0.5 NTU.

The instantaneous  peak operating  flow for the plant
was established at 16 Us (0.36 mgd) for  each of the
two plants,  or 32  Us (0.72  mgd) for the total  plant.
This flow is  based on a review of flow records for the
previous year and the practice of only  operating one
of the raw water pumps. On days the plant  operates
for longer than 8 hr, the treatment  processes are still
operated  at  a maximum  flow rate of  32  Us  (0.36
mgd).

The flocculation basins were  rated at 48 Us (1.1) mgd
for the total  plant. Most of the flocculation capabilities,
however,  are provided  by  the "new" plant.  The two
flocculators  were rated at  39 Us (0.90 mgd),  under
the assumption  that the horizontal perforated  baffles
would be replaced and the  mechanical mixers  made
operational.   The flocculation  portion  of the  "old"
plant's  solids contact clarifier was rated at 8.3 L/s
(0.19 mgd).

For sedimentation, the  solids contact clarifier was
rated at 14 L/s (0.32 mgd) and the combined package
plants at 17 L/s  (0.38 mgd) for a total plant capacity of
31 L/s (0.7 mgd). The shallow depth and configuration
of the solids  contact clarifier were judged to limit  its
capacity.  Higher surface overflow rates were applied
to the package plants because of the tube settlers.

Total filtration capacity  for the plant was rated at 53
L/s (1.2 mgd). A filter loading rate  of 117 m3/m2/d (2
gpm/sq  ft)  was  used for  the  "old"   plant,  which
resulted in a rated capacity of 16 L/s (0.36 mgd). The
filters on the "new" plant were rated at  35  L/s (0.79
mgd) based  on a loading  rate of 293 m3/m2/d  (5
gpm/sq  ft).  These ratings  assume the  rate  control
valves on both plants will be  operational.

The  disinfection system  was rated  at  18  L/s (0.42
mgd). Future drinking water regulations  for disinfection
will be  based  on CT  values  needed  for various
 removals of Giardia  cysts and inactivation of viruses.
To establish  the  CT required, it  was assumed the
 plant's disinfection system would have  to provide 1.5
 logs  of cyst removal  with 2.5 logs of removal credited
for the other treatment processes.  The total of  4 logs
 of cyst removal  required  was  based on  the CPE
 team's estimate of the quality of the raw water.
                                                    89

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 Figure 4-60.  Plant 12 performance potential graph.


     Unit Process
                                             0.2
                                                         0.4
                      Flow, mgd

                         0.6
                                                                                 0.8
                                                                                             1.0
                                                                                                         1.2
     Flooculatfon'
       Ok) Plant HOT, min

       New Plant HOT, min

       Total


     Sedimentation2^
       Old Plant SOR, gpm/sq ft

       New Plant SOR. gpm/sq ft

       Tola)


     FIItrationซ.s

       Old Plant HLR, gpm/sq ft

       New Plant HLR, gpm/sq ft

       Total


     Disinfection6
       HOT, min
 90
0.43
 1.3
 1.1
1.3
                                             85
             45
                         30
            2.5
                        3.8
                                                         42
                                     23
                                          Peak Instantaneous Operating
                                               Flow = 250 gpm
                        Peak Instantaneous Operating
                            Flow = 500 gpm
   1 Rated at 20-min HOT - assumes baffles reinstalled and functional micers in new floe basin.
   2 Old plant rated at 0.7 gpm/sq ft - shallow depth and configuration considered limiting.
   3 Now plant rated at 2.5 gpm/sq ft - tube settlers allow higher rates.
   * Old plant rated at 2 gpm/sq ft - integrity of tanks was assumed to be adequate.
   5 New plant rated at 5 gpm/sq ft - assumes rate control valves are operational.
   8 Rated at CT = 100 with 2.5 mg/L chlorine dose, which requires a 40-min HOT; allowed 10 percent of available volume for contact
    time, temperature s 5ฐC, pH = 7.5, 4-log required reduction, 2.5 log allowed for plant if operated well.
To achieve  the 1.5  logs  of cyst removal,  the CPE
team  estimated that the  disinfection system  would
have to provide a  CT  of  100. This  CT  value is  for
chlorine at a 2.5 mg/L dose, pH 7.5, and  temperature
of SO. The contact time was based on  the chlorine
being  added  ahead of the  "new"  clearwell  and the
flow passing through  both  clean/veils.  Only 10 percent
of the theoretical detention time in the clearwells was
used  because  the clearwells  are  not  baffled and
because they are subjected to fill and draw operation.
The piping arrangement, which does not assure that a
flow passes through both  clearwells,  also  contributed
to this rating. The actual levels of disinfection required
for the plant in the future will be determined by the
State. The estimates  in this  CPE of the required total
number of log reductions and the  allowances for
actual contact  times in the  clearwells may change
when final regulations are developed.

The performance potential graph shows  that, on  a
total plant basis, the major  unit  processes have  a
             rated  capacity  close  to  or  exceeding  the  peak
             instantaneous  operating flow  of 32  Us (0.72 mgd),
             with  the  exception  of the  disinfection  process.
             Flocculation is adequate up to 48 Us (1.1 mgd) if the
             flocculators on  the  "new"  plant  are returned  to  their
             original condition.  The  sedimentation processes  are
             projected adequate to  treat a  flow of  31  Us  (0.70
             mgd),  which is  borderline. The filtration  system, rated
             at 53 Us (1.2 mgd), was rated considerably more than
             adequate to treat  the  peak instantaneous  operating
             flow. Lack of baffling  in the clearwells and the piping
             arrangement between the  two  clearwells limited  the
             projected capacity of the disinfection process.

             On an individual plant  basis, the performance potential
             graph  shows that  both plants  do not have equal
             capabilities. For the total plant  to have a rating of 32
             Us (0.72 mgd), more than half of the flow will  have to
             be  treated  in  the   "new"  plant. The solids  contact
             clarifier on the  "old"  plant limits the  flow  it  can
             adequately treat to 8.3 Us (0.19 mgd).
                                                      90

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 Performance Assessment
 Figure 4-61  shows  the finished water  turbidity  as
 reported by the plant staff for a 12-month period. The
 current State  regulation for turbidity  is 1.0  NTU. The
 federal SWTR will require the plant to meet  a 0.5-NTU
 finished  water turbidity  95 percent  of the  time. The
 plant generally complies with the 1.0-NTU  regulation,
 but is consistently above the 0.5-NTU required by the
 SWTR. A probability plot of this  same data, shown in
 Figure 4-62, indicates that under present  conditions
 this  plant  would  only  meet  0.5 NTU less than  10
 percent of the time.

 During the  CPE,  special  studies were conducted to
 assess the performance of both  the  "old" and "new"
 filters after backwashing. With adequate  facilities and
 operation of proceeding unit  processes, a properly
 operated filter should  produce a  finished  water
 turbidity  of  approximately  0.1  NTU and only
 experience a 0.2-NTU rise in turbidity in the finished
 water for  approximately  10  minutes  after  being
 restarted following  backwashing.  For  this  special
 study, both filters were  sampled  for  a  30-minute
 period after being restarted following backwashing.

 Figure 4-63 shows the results for the "old" filter. Prior
 to backwashing, this filter was  producing  0.22-NTU
 water. After backwashing, however.the  water  quality
 peaked  at  38 NTU after 1 minute and did not drop
 back  to  the original  value even  after 30 minutes. A
 turbidity  of 1.0 NTU  was not achieved for  almost 20
 minutes. Figure  4-64  shows   the results  after
 backwashing  one of  the "new"  filters. Prior  to
 backwashing,  the filter  was  producing   a  12.5-NTU
 water, significantly  above  the  1.0-NTU regulation.
 After  backwashing,  the  water quality improved,  but
 had not achieved adequate performance even after 20
 minutes.

 These results indicate a significant performance
 problem  that may be attributed to the filters or to  the
 fact that  the water being applied to  the filter has  not
 been properly  treated  and conditioned  in  the
 preceding unit processes. During the  backwash of  the
 "new" filter, large amounts  of  air  were  observed
 bubbling  up through the media.

 During  the two  special  studies,   the  team also
 collected samples of the finished   water  from the
 clearwells.  These results, shown  in Figure 4-65,
 indicated that significantly high levels  of turbidity were
 passing into the city water systems; well above the
 levels allowed by the  State.  Such high  levels  of
turbidity pose a significant  health  risk to  the
 community.

 Performance-Limiting Factors
 The  factors identified as  having a  major  effect  on
 performance  on  a long-term  repetitive  basis  were
 prioritized and  are summarized below:
 1.  Performance Monitoring - Operation:  The practice
    of sampling at optimum times, though allowed by
    current regulations, has resulted in an  inaccurate
    assessment of  the  plant's true performance.
    Accurate monitoring would  have alerted the plant
    staff to the serious performance problems  at the
    plant and likely would have resulted  in regulatory
    pressure to  correct them.  Improperly operating
    laboratory  instruments used for  monitoring also
    led to an improper interpretation of performance.

 2.  Plant  Administrator's  Policies  -  Administration:
    Current and historical actions by the mayor  and/or
    city council were  inadequate in  recognizing the
    significance of  poor  water  quality  and
    inappropriate in  that  they  did  not aggressively
    address the causes of the  situation.  The existing
    new plant,  constructed in 1977, had been allowed
    to deteriorate. Repairs and maintenance to protect
    system integrity  had  been largely ignored. Staff
    with expertise in  water treatment were performing
    numerous  other city  functions away  from  the
    water plant, and staff with  virtually no  training in
    water treatment were  manning  the plant  for only
    portions  of  the time  it was  operating.  "Muddy"
    water was accepted as a way of life. Agreements
    to provide  water to   other  communities  were
    negotiated  and perpetuated despite the increased
    demand  that was  placed on a  marginally
    functioning system. A  significant change in past
    policies and in emphasis on the  water plant will be
    necessary  to reduce  the  health  risk associated
    with current water plant performance.

3.  Maintenance: Years   of  neglect of  all  plant
    equipment  have  degraded  a  potentially  well-
    equipped plant to essentially a nonfunctional  state.
    Considerable expenditures  will be  required  to
    make  this  equipment  operational  and to keep it
    maintained.

4.  Water Treatment Understanding - Operation: The
    plant staff  demonstrated  a  significant  lack  of
    understanding of  even basic concepts of  water
    treatment, allowing the water to  cascade onto the
    filter  media,  starting dirty  filters, performing no
    process control  testing, and essentially providing
    no adjustment of chemical feed rates. There was
    also a  lack of urgency to  repair and/or  replace
    improperly  functioning  equipment  essential  to
    providing  water treatment.

5.  Process Control  Testing -  Operation: A process
    control testing program to  optimize unit process
    performance did  not exist at the plant. Process
    control testing is  essential for water plants served
    by surface  sources because  of the frequent and
    rapid  changes  in raw  water quality. Basic
    equipment was available to  conduct  this  testing,
    but was not used.
                                                  91

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Figure 4-61.  Finished water turbidity profile - Plant 12.

              i i i i  | i i i  i | i i  i i | i  i i i | i i i  i | i i
         ID

         OJ
     :D

     ซc  m
                                                                                                  Present
                                                                                                Requirement
                                                                                                  Future
                                                                                                Requirement
             i  i i i I  i i I i  [ i I i  i | i i  i i [ i  i i i  | i i i  i | i i  i i [ i  i i i I  i i i i |  i i i i  | i i i  i | i  i i i |  i i i i

         SEP88  OCT   NOV   DEC  JRN89  FEE   MRR  RPR   MRY   JUN   JUL   RUG   SEP   OCT
Figure 4-62.  Probability plot of finished water turbidity - Plant 10.
          in
           ป
          ru
          OJ --
          in
          (S)
             1         1
10               50

        Probability
90
99      99.9
                                                     92

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Figure 4-63. Old  plant north filter effluent turbidity profile
           after backwash - Plant 12.

  Turbidity, NTU

     40  r-
                                  Present Requirements
                           15     20

                          Minutes
Figure 4-65.  Clearwell turbidity profile after filter backwash
            Plant 12.
 Turbidity, NTU

   8  r-
                      Present Requirements


                     J	I	I	
          10    20    30    40    50    60

                         Minutes
                                                                                                     J
                                                                                                      70
Figure 4-64.  New plant north filter effluent turbidity profile
            after backwash - Plant 12.
  Turbidity, NTU

     12f
          Present Requirements
                           I
                           10

                         Minutes
                                     15
                                              20
6.  Filtration  -  Design*: This factor has an  asterisk
    because  of the air observed  above  the  filters
    during  backwash.  Air entering the  filters during
    backwash may have  disturbed the filter media to
    the  point  that  it will have to be replaced. The
    condition of the filter media was not verified during
    the  CPE. The filter tanks  on the "old" plant are
    severely corroded  to the point that they could fail
    entirely.

7.  Disinfection - Design*: This factor has  an  asterisk
    because  it was  assessed based on the  initial
    disinfection requirements of the new regulations.
    These requirements  may  change  when  final
    regulations are developed by the State.  On  this
    basis,  however,  inadequate  contact  time is
    provided  because  of  a lack of baffling in  the two
    clearwells and  a lack of piping  to allow  them to
    operate in series.

Factors identified as having either a minimal effect on
a routine basis, or a major effect on a periodic basis
are summarized below in  order of priority.

 1.  Staff Number - Administration: Additional  staff are
    required  to provide  adequate coverage of the
    plant, to perform  the  necessary  process control,
    and to complete maintenance functions.

2.  Staff Qualification  - Administration: All of the plant
    staff must  have high levels of education  to make
                                                      93

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    proper operation  and maintenance decisions; all
    staff should also be certified.

3.  Process  Flexibility  -  Design: The capability  is
    needed to feed polymers and filter aids at different
    locations in the  plant to optimize performance.
    This will be especially  critical  if the plant  is to
    consistently meet a required finished water quality
    of 0.5 NTU.

4.  Alarm Systems - Design: The  plant experiences
    rapid  variations in raw  water quality  and has a
    limited number of  operations staff present to make
    necessary  adjustments  in  response to these
    variations (e.g., adjust chemical  or chlorine doses,
    or correct problems with key process equipment).
    On these occasions,  process performance could
    degrade to a  point where  it poses  a  potential
    health  risk to  the  city. A  turbidity  monitoring
    system tied to raw and  finished  water and  a
    chlorine residual monitoring system could  be  used
    to alert the  plant staff to process problems before
    finished water quality reached undesirable levels.

5.  Flow  Proportioning  to  Units  - Design:   Flow
    measurement  and  flow  control  devices  are
    needed to accurately split flow to ensure that  each
    plant  receives the  proper  flow  rate.   This is
    especially critical  because the flow to the "old"
    plant  must be  limited  to achieve   desired
    performance.

6.  Flocculation -  Design: In  the "new" plant,  the
    flocculator's original  horizontal perforated baffles
    will have to be  replaced and  the mechanical
    mixers made  operational.  The flow to the  "old"
    plant must be  limited  because of the  size of the
    flocculation  section of the solids contact clarifier.

7.  Sedimentation  -   Design:  The  sedimentation
    capabilities  of the plant  are  marginal because of
    the shallow depth of the  solids contact clarifier
    and the limited surface area  of the sedimentation
    sections of the  package plants.
The amount of bond  indebtedness  of  the  city was
considered a minor factor, because it could limit the
ability to properly fund operation and maintenance or
needed  repairs to  the plant.  Practices  used  for
disposal of  plant  sludges  were  not  considered
environmentally  sound,  but had no  impact  on plant
performance. A lack of simple taps on all of the filters
prevented proper monitoring of filter performance.

Projected Impact of CCP
Data  collected  during the CPE  indicated severe
performance problems. Correcting  the identified
factors  would  appreciably  improve  the  plant's
performance  and allow it to  meet both  current and
future regulations. As  such, implementation of a CCP
represented a viable option for the plant.
                                                  94

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Plant 13

Facility Description
Plant 13 is a conventional  water treatment plant that
supplies water to the city for domestic use. Its source
is a  nearby river.  Based on a review of plant records
for the year, the peak flow was 66  Us (1.5 mgd). The
plant includes  the  following  unit  processes  and  is
shown schematically in Figure 4-66:

• Raw water intake structure and two vertical turbine
  60-hp, 65-L/s (1,040-gpm) pumps

ซ Orifice  plate with a totalizer-recorder to  measure
  raw water flows

• Five  volumetric chemical feeders: one each  for
  alum,  lime,  soda ash,  potassium  permanganate,
  and powdered activated carbon

• Mechanical 3-hp flash mixer

• Two dual-stage  flocculation basins. Each stage is
  4.9-m (16-ft) square and  3.7-m (12.2-ft)  deep. Each
  stage  contains  a  vertical paddle  flocculator
  operated from a central 1 -hp variable speed drive

• Two sedimentation basins  11 m (36  ft) long and
  6.1 m (20  ft) wide, containing 60ฐ tube settlers  11
  m x 4.5 m  (36 ft x 14.7 ft) and 3.7-m (12.2-ft) deep.
  Each basin has a weir length of 43.9 m (144 ft)

• Two mixed media filters 3.4 m x  3.8 m (11 ft x 12.3
  ft) fitted with rotary surface wash, and  containing 84
  cm (33 in)  of media

• Backwash  water  and settling basin sludge  decant
  basin

• Four sludge drying beds

• Diaphragm metering pump to feed hydrofluosilicic
  acid

• Vacuum-controlled solution  feed  pre-/post-
  chlorination system  fed from  68-kg  (150-lb)
  cylinders

• Two 575,300-L  (152,000-gal) clearwells

• 189-L/s (3,000-gpm)  vertical  turbine  backwash
  pump

• Two  vertical turbine high-service pumps  with a
  capacity of 66 L/s (1,050 gpm)

• 6,340-L (1,675-gal) wet well for  the backwash and
  high-service pumps

Water  is taken from the river through  any of three
intake  pipes  located at different depths.  The intake
pipes supply water to a wet well. Either of two vertical
turbine pumps  is used to supply raw water from the
wet well to the  plant. The plant is usually operated 17-
20 hr/day.  Higher demands are  met by operating the
plant for longer periods.

An  orifice  plate measures raw  water flow rates just
prior to chemical addition.  Flow rates are charted on a
totalizer-recorder located on a panel with the reservoir
level alarm system.

Chlorine is injected prior to lime and alum addition at
concentrations  high  enough  to  maintain  a  1.5-mg/L
residual on top of the filters  - 45  kg (100 lb)/d.  The
rate  is  changed only  when "muddy"  waters  are
observed at the plant influent.

Alum  and  lime  are added  using  dry  volumetric
feeders.  Alum  and  lime  slurries are  prepared  by
adding dry chemicals to  mixing tanks beneath the
feeders and conveyed by  gravity to a trough carrying
raw water  to the  rapid mixer. Volumetric  feeders are
also  in place  to feed  potassium  permanganate,
powdered activated carbon, and soda ash slurries to
meet seasonal variations in raw water quality.

Alum  feed rates are  adjusted  based  on visual
inspection  of  the  floe  particles  in  the  flocculation
basins. A jar testing apparatus is in place,  but is  used
infrequently (10-15  times/yr).  The lime feeder is
currently operating  at maximum output,  and is not
adjusted.

The chemical  slurries and raw  water enter  a 0.9-m
square (3-ft square) and  2.4- m (7.8-ft)  deep basin
containing a mechanical flash  mixer.  The basin has a
hydraulic  detention time of  30  seconds. The  CPE
team  calculated the  G value for the  mixer to  be
adequate at 894 sec-"1.

After  exiting the  rapid mix  basin  the water  splits
hydraulically and  flows through  a parallel   train of
identical flocculation, sedimentation, and filter basins,
prior to entering the two clearwells.

The coagulation/flocculation process is performed  in a
dual stage  system; each stage is fitted with horizontal
paddles. A pair  of variable speed  motors, one for each
stage, drives a central shaft  which in turn drives the
paddles for each stage of the  parallel trains. Each
basin  has  a detention time of 45 minutes  and a peak
G of 77 sec-"".

Flocculation basin effluent  is directed to the bottom of
the  two pairs  of sedimentation  basins and  flows  up
through a  set of 60-degree tube  settlers. Each of the
two basins has a detention time of 2.1 hr.  The basins
have a combined surface overflow rate of  58 m3/m2/d
(1,420 gpd/sq ft).  Sludge  is  manually removed
approximately  every  2 months  and washed to  a
decant basin.  Originally, decant  from the basin was
                                                  95

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Figure 4-66.  Plant 13 process flow diagram.
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recycled to the head of the plant, but the  recycle
pump is out of service so the decant is discharged to
the river. Sludge from the decant basin is washed to
the drying  beds for ultimate discharge to  a sanitary
landfill.

Settled  water then enters a pair of mixed media filters
through metal troughs above 12.6 m2 (136 sq ft) of
media.  Filter flow  rates  are  controlled  by  raw water
pumping  rates, which  in  turn  actuate pneumatic
valves,  maintaining an approximate loading rate of 222
m3/m2/d (3.8 gpm/sq ft).

Backwash  frequency  is determined  by measuring
headless across the filters or by observing a rise of
clearwell turbidity.  Filter  runs are routinely 40-45 hr.
Backwashing  routinely consists of  6-7 minutes of
surface wash at a rate of 26 m3/m2/d (0.45 gpm/sq ft).
The media beds are then washed at a rate of 1,055
m3/m2/d (18 gpm/sq ft) for an indiscriminate duration.

The influent troughs  are  then used  to  discharge
backwash water to the decant basin.  The filters are
capable of filter-to-waste operation,  although this is
not commonly practiced.

Chlorine (23 kg [50  lb]/d), hydrofluosilicic acid (91  L
[24  gal]/d), and, occasionally,  soda  ash are  then
added  to  filtered  water  prior  to  entering  the  two
clearwells.  Each clearwell has  a hydraulic detention
time of 4.9 hr. Current  piping  configurations  do not
permit operating the clearwells in series.

Finished water then flows  into  the wet well which
supplies water for the two high-service pumps, as  well
as the backwash pump.

Major Unit Process Evaluation
The performance potential graph  is shown in Figure 4-
67. The shortest bar represents the treatment process
limiting  the  plant's  capacity  to  achieve the  desired
performance of less than  0.5 NTU.

The instantaneous  peak operating  flow  was
established 66 L/s (1,050 gpm). This  is based on a
review  of flow records for the previous year  and the
practice of  only  operating  one of the  raw water
pumps.  The plant is normally operated approximately
17-20 hr/day.  To  meet  events  of  peak water  use
during the  summer,  the  plant is operated 24  hr/day.
On those  days the treatment  processes  are  still
operated at a maximum flow rate  of  66 L/s (1,050
gpm).

The flocculation basins  were rated  at 149 L/s  (3.4
mgd) based on a 20-minute  hydraulic  detention  time
and two-stage  flocculation with a variable speed input.

Due to  the use of  tube settlers, the sedimentation
basins  were rated  at 101 L/s (2.3 mgd) based on a
surface  overflow rate of 88 m3/m2/d (1.5 gpm/sq ft).
 Filtration capacity for the plant was  rated at 85  L/s
 (1.95 mgd) based on the state maximum allowable
 loading rate of 293 m3/m2/d (5 gpm/sq ft).

 The disinfection  system  was  rated  at  26 L/s  (0.6
 mgd). Future drinking water regulations for disinfection
 will  be based  on CT values  needed for various
 removals of Giardia cysts and inactivation  of viruses.
 To establish the CT required, it was assumed that the
 plant's disinfection system would have to provide  1.5
 logs of cyst removal with 2.5 logs of removal credited
 for the other treatment processes. The total of 4 logs
 (99.99 percent) of cyst removal required for Plant 13
 was based on the CPE team's estimate of the quality
 of the raw water.

 To achieve the  1.5 logs of cyst removal the CPE team
 estimates that the disinfection system would have to
 provide a CT of 183. This  CT value is for chlorine at a
 2.5 mg/L dose, pH 8.0, and temperature of 5ฐC. The
 contact time was  based exclusively on  the  post-
 chlorine dose.  Only  10  percent of  the theoretical
 detention time in the clearwells was used because  the
 clearwells  are  not baffled and  thus are  subject to
 hydraulic  short  circuiting.  The actual  levels of
 disinfection required for the plant in the future will be
 determined by the State. The estimates in this CPE of
 the required number of log reductions of Giardia  cysts
 and viruses  and  the  allowances for  actual contact
 times  in  the clearwells  may  change  when  final
 disinfection regulations are developed.

 Raw and finished water pumping capacity was rated at
 66 L/s (1.5 mgd).  This rating was based on use of a
 single raw/finished water pump with one pump out of
 service.

 As shown  in the performance  potential  graph, the
 major unit processes have a rating capacity exceeding
 the  instantaneous peak  operating flow,  with  the
 exception  of the disinfection process. Again, the lack
 of  baffling  in the clearwells  limited  the  projected
 capacity of the disinfection process.

 Performance Assessment
 Figure  4-68  shows  the settled  water turbidity
 measured by the plant staff  over  the  previous 12-
 month period. Settled water turbidities were generally
 less than 2.0 NTUs, although there were also several
 periods  of higher turbidity.  These  appeared  to  be
 related  to periods  of high  raw  water  turbidity,
indicating that chemical feed  rates were  not properly
adjusted to compensate for the changes in raw water
turbidity.

 Figure 4-69 shows the finished water turbidity reported
over the previous  12 months. Current regulations  for
finished  water  turbidity are   1.0  NTU.  Future
regulations will  require the plant to meet a 0.5-NTU
finished water turbidity 95  percent of the time. Except
for several days in the first 3 months, the plant met
                                                  97

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Figure 4-67.  Plant 13 performance potential graph.


    Unit Process
                                           1.0
            Flow, mgd
            2.0         3.0
                                                                              4.0
    Flocculatlon1
      HOT, min


    Sedimentation2
      SOR, gpm/sq ft


    Filtration*
      HLR, gpm/sq ft


    Disinfection4
      Contact time, min


    Raw/Finished PumpingS
 68
0.66
2.6
                                           694
            34
                        23
            1.3
                                         Peak Instantaneous Operating
                                         Flow (1 Pump) = 1,050 gpm



   ' Rated at 20 -min HOT - based on 2-stage with variable energy input.
   2 Rated at 1.5 gpm/sq ft - based on tube settlers with annual sludge removal.
   3 Rated at 5 gpm/sq ft - based on State maximum allowable loading.
   4 Rated at CT * 183 with 2.5 mg/L chlorine dose, which requires a 73-min HOT; allowed 10 percent of available volume for contact
    time, temperature * 5ฐC, pH = 8, 4-log required reduction, 2.5 log in plant, 1.5 log disinfection.
   5 Assumes firm capacity at 1.5 mgd with one pump out of service.
the 1.0-NTU turbidity requirements and was regularly
below the  0.5-NTU  required by the SWTR. Figure 4-
70 presents  a probability plot  of this data  and shows
that  the plant produces a finished water  turbidity of
less  than  0.5  NTU  approximately 70  percent of the
time. Comparing Figures 4-68 and 4-69 reveals  that
higher finished water  turbidity occurred  during  the
same periods that  the settled  water  turbidity was
above 2.0  NTUs,  providing  further  evidence that
chemical feed rates were  not  properly adjusted when
raw water turbidities changed.

During  the CPE,  a special study was conducted to
assess  the  performance  of   the   filters  after
backwashing. With adequate facilities and operation of
preceding  unit processes,  a  properly operated filter
should  produce a finished  water  turbidity  of
approximately  0.1 NTU and experience only a  0.2-
NTU rise  in  turbidity in  the finished  water for
approximately 10  minutes after being  restarted
following backwashing.  For this special study, finished
water from  Filter 1  was  sampled for  a  40-minute
period after being restarted following backwashing.
             Figure 4-71  shows  the results of this  special study.
             Prior to  backwashing, the filter  was  producing  1.0-
             NTU water.  After backwashing,  the turbidity levels
             increased to 3.6 NTU and did not stabilize at the 0.1-
             NTU level for  30 minutes.  The  special  study   also
             found a  problem with  an  inadequate amount of
             backwash water flow at the beginning of the backwash
             cycle. A period  of essentially no flow was followed by
             a violent eruption of  the filter media as the backwash
             water finally started  entering  the  filter.  Further
             investigation of the  problem revealed that the  valve
             that controls the backwash water flow  was  sticking in
             a closed position and would finally snap fully open.

             These results indicate that a finished water that meets
             current and  future  regulations is  usually  produced.
             During periods  of high raw water turbidity,  it appears
             that the plant staff is not adequately adjusting process
             control to  allow the plant  to  produce  a consistently
             good quality finished water. Turbidity levels following
             backwashing also indicate that better process control
             could  be  practiced  to  limit  the  passage  of  high
             turbidity  water  into  the distribution system following
             filter backwash.
                                                     98

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Figure 4-68.  Settled water turbidity profile - Plant 13.
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           DEC JRN89 FEE  MRR  RPR  MRY  JUN  JUL  RUG  SEP  OCT  NOV  DEC JHN90
Figure 4-69.  Finished water turbidity profile - Plant 13.
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                                                                                          " T Requirement
                                                                                              Future
                                                                                            Requirement
          DEC JRN89 FEB  MRR  RPR  MRY  JUN  JUL  RUG  SEP  OCT  NOV  DEC JRN90
                                                  99

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Figure 4-70. Probability plot of finished water turbidity - Plant 13.
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                             50
                        Probability
                            99      99.9
Figure 4-71. Filter effluent turbidity profile after backwash
           Plant 13.

TurbKiity, NTU

   4  i-
   0
                10
  20
Minutes
                                    30
                                             40
Performance-Limiting Factors
The  following  factor was identified as having a major
effect on a long-term repetitive basis:

1.  Disinfection  - Design*:  This factor has an asterisk
    because it  was  assessed based  on  the initial
    disinfection  requirements of new  regulations.
    These  requirements  may change  when  final
    regulations are  developed by the State. Using this
    basis,  however,  inadequate  contact  time  is
    provided because  of a lack of baffling  in the two
    clearwells and  a lack  of  piping to allow them  to
    operate in series.

Factors identified  as  having  a minimal  effect on a
routine  basis, or a  major  effect on  a periodic basis
were prioritized and are summarized below:

1.  Supervision  - Administration: The plant has 24-hr
    coverage, which requires  a large staff. This large
    staff  works without  any formal  organizational
    structure,  no lines of authority, no  chief operator,
    and a total lack of leadership. With this  absence
    of  supervision, essentially   no communication
    occurs  between the staff on  the different shifts.
    There are no regular  meetings, no operating log,
    and no  shift overlaps where  essential information
    on  the  status  of  the  plant  can be discussed.
    Without this essential supervision, the productivity
    of the plant staff is poor, which encourages poor
                                                    100

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    performance.  For  example, the alum feeder that
    needed repair at the end of the first shift was not
    repaired during either of the next two shifts. Lack
    of  supervision and  communication were made
    worse  by a  total lack of  standard  operating
    procedures.

2.   Application of Concepts and  Testing to Process
    Control  -  Operation: While  the  plant staff is
    certified and has a knowledge of water  treatment,
    they  are not  able to apply  their  knowledge  to
    properly  control  the treatment processes  to
    optimize performance.  Filter-to-waste capabilities
    at the plant are not used to minimize the passage
    of high turbidity water to the clearwells  after filter
    backwash. The plant was also  operated for a
    month without a turbidimeter. Iron and manganese
    levels were high in the finished water on several
    occasions, but no  process changes were initiated
    by the plant staff. Lime is fed at the same point as
    the alum even though the  lime raises the pH out
    of the optimum range for alum coagulation.

3.   Process Control Testing - Operation:  A process
    control testing program to optimize unit process
    performance did not exist.  Process control testing
    is essential for water plants served by  surface
    sources because of the  frequent and  rapid
    changes in raw water quality.  Basic  equipment
    was available  to conduct this testing, but was not
    used.

4.   Preventive Maintenance -  Maintenance: The lack
    of a  maintenance  program has resulted in  many
    key  pieces of  equipment needed for  optimal
    operation not  operating  or  near  failure.  Filter
    controls, the  influent control  valve, the finished
    water flow  meter, and backwash  water  reclaim
    pumps are not operating.  New alum  and  lime
    feeders were  not installed to replace the marginal
    units still in  operation. Backwash  control  valves
    were  malfunctioning and the  drives on  the
    flocculators were making excessive noises with no
    indication of repairs being planned.
5.  Water Demand - Administration*: This factor  has
    an asterisk  because  it  is  projected that in  the
    spring of  1990 the water  demands of  the new
    industry and development in the city will exceed
    the raw water pumping capacity of the plant. Plant
    administrators  committed the  plant to supply  this
    water with  little  regard to  its impact on  the
    capacity or performance  of the  plant.

Several of the administration's policies are considered
to have  a  minor impact on  the performance of  the
plant. Current  rate structures do not allow the plant to
be self-sustaining and cover all needed operation  and
maintenance costs. There is a total lack of long-range
planning to allow for growth within the community so
as  to  minimize impact  on  plant's  capacity and
performance.  Funding for the plant is  also  kept low,
preventing  repair  of key equipment.  Other factors
thought to  have a minor impact on performance  are
the low pay of the plant staff as  compared to other
plants in the State and the lack of process flexibility.

Projected Impact of a CCP
Data collected during the CPE indicated that  this plant
usually  performs satisfactorily, with some  problems
responding to  changes  in raw water  turbidity.
Correcting  the identified  factors  would  appreciably
improve  the consistency of the plant's performance
and  allow  it to  meet  both current  and  future
regulations. As  such,  implementation  of  a CCP
represented a  viable option for this  plant.
                                                  101  *U.S.GOVERNMENT PRINTING OFF ICEI 1 990-74 8-159/004 I 2

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