600281168

                                        September 1981
DEPLOYMENT CONFIGURATIONS FOR IMPROVED OIL
  CONTAINMENT WITH, SELECTED SORBENT BOOMS
                        by
                   Gary F. Smith
         Mason & Hanger-Silas Mason Co., Inc.
             Leonardo, New 3ersey 07737
             Contract Number 68-03-2642
                   Project Officer

                   John S. Farlow
        Oil and Hazardous Materials Spills Branch
 Municipal Environmental Research Laboratory-Cincinnati
              Edison, New Jersey 08837
MUNICIPAL ENVIRONMENTAL RESEARCH LABORATORY
      OFFICE OF RESEARCH AND DEVELOPMENT
     U.S. ENVIRONMENTAL PROTECTION AGENCY
              CINCINNATI, OHIO 45268

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                                 DISCLAIMER
      This  report  has been  reviewed  by  the  Municipal  Environmental  Research
Laboratory, U.S. Environmental  Protection  Agency, and  approved for publication.
Approval does not signify that the contents necessarily reflect the views and policies
of the U.S. Environmental Protection Agency, nor does mention of  trade  names or
commercial products constitute endorsement or recommendation for use nor does the
failure to mention or test other commercial products indicate that other commercial
products are not available or cannot perform similarly well as those mentioned.
                                        ii

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                                  FOREWORD
      The U.S. Environmental Protection Agency was created  because of  increasing
public  and government  concern about the  dangers  of  pollution to  the health  and
welfare of the American people. Noxious air, foul water, and spoiled land  are tragic
testimonies to the deterioration of our natural environment.  The complexity of that
environment and the interplay of its components require a concentrated and  integrated
attack on the problem.

      Research and development is that necessary first step in problem solution; it
involves defining the problem, measuring its impact, and searching for solutions.   The
Municipal Environmental Research Laboratory  develops new and improved technology
and systems to prevent, treat, and manage wastewater and solid and hazardous waste
pollutant  discharges from  municipal and community sources, to preserve  and treat
public drinking water supplies, and to  minimize the adverse economic, social, health,
and aesthetic effects  of pollution.  This publication is  one  of  the products of that
research and provides  a most vital communiations link between the research and the
user community.


      This report describes full-scale testing of three  sorbent commerical oil spill
booms.  Based on the results presented here, more efficient operating techniques for
booms used in water currents can be developed.  The  methods, results, and techniques
described are of interest  to those  interested in specifying, using, or testing  such
equipment.   Further information may  be obtained through the Solid and  Hazardous
Waste  Research Division,  Oil  and Hazardous  Materials  Spills  Branch, Edison,  New
Jersey.


                            Francis T. Mayo, Director
                   Municipal Environmental Research Laboratory
                                   Cincinnati
                                        ill

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                                 ABSTRACT
      Performance  tests  on three catenary  oil containment configurations  using
sorbent booms sections alone and in conjuction with a conventional containment boom,
were  conducted at the U.S. Environmental  Protection  Agency's  Oil and  Hazardous
Materials Simulated  Environmental Test  Tank (US  EPA OHMSETT).   Other  test
variables included wave condition, tow speed, and oil quantity encountered. Maximum
no-oil-loss  containment tow  speed was determined  for  each  wave and oil  quantity
tested.

      The  use of  an all sorbent boom with a multi-layer sorbent  raft at the apex
exhibited average increases in no-oil-loss tow speed of 0.13 m/s over previous results
using a single layer boorn in calm water.

      Use  of a sorbent raft inside the apex  of  a conventional  containment  boom
increased turbulence and caused oil loss at lower speeds  than use of the conventional
boom alone.  No-oil-loss tow  speeds using the sorbent boom raft at the boom apex also
decreased from previous results using a single layer sorbent boom in  the 0.3-m harbor
chop  wave.  Loss  was  due to increased turbulence from raft sections striking each
other from  the wave action.

      Recovery of sorbed fluid  and regeneration  of  the boom sections was unsuc-
cessfully attempted using a commercially available sorbent and wringer.

      This report was submitted  in fulfillment  of Job Order No. 49, Contract No. 68-
03-2642, by Mason & Hanger-Silas Mason Co., Inc., under the  sponsorship of  the U.S.
Environmental Protection Agency.  This report covers the period  12 through 16 June
1978 with work completed 22 September 1978.
                                       iv

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                                   CONTENTS


Foreword 	    iii
Abstract  	    iv
Figures and Tables  	    vi
Conversion Factors	    vii
Abbreviations	    viii

       1.     Introduction	      1
       2.     Conclusions and Recommendations	       2
       3.     Materials	      4
       4.     Experimental Procedures	      8
       5.     Results and Discussion	    13

Appendix

             OHMSETT  Description	     21

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                                   FIGURES
Number
2
3
4
5
6
7
8
Regeneration of saturated boom sections using a
      Petro-Trap wringer	
3M Company Type 270 sorbent boom	
Conwed Corporation heavy duty sorbent boom . .
Regeneration of oil-soaked boom sections	
Typical assembly of Petro-Trap wringer rollers .
Boom configuration for Phase A testing	
Boom configuration for Phase B  testing,
                                                	     3
                                                	     5
                                                	     5
                                                	     6
                                                	     7
                                               	     9
                                               	    10
Boom configuration for Phase C testing	    12
                                   TABLES
Number

1
2
3
1
5
6
7
8
Sorbent Boom Specifications	
Results of Added Rows to Sorbent Raft ....
3M Company Type 270 Sorbent Boom Results
3M Company Type 270 Sorbent Boom Results
3M Company Type 270 Sorbent Boom Results
Conwed Sorbent Boom Results	
Conwed Sorbent Boom Results	
Conwed Sorbent Boom Results	
                                                             15
                                                             16
                                                             17
                                                             18
                                                             19
                                                             20
                                      VI

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                             LIST OF CONVERSIONS
METRIC TO ENGLISH

To convert from

Celsius
joule
joule
kilogram
metre
metre-
metre-
metre,
metre..
metre
metre/second
metre ^econd
metre ../second
metre ,/second
metre  /second
newton
watt

ENGLISH TO METRIC

centistoke
degree Fahrenheit
erg
foot-
footZ
footAninute
foot /minute
foot-pound-force
gallon (U.S. liquid)
gallon (U.S. liquid)/minute
horsepower (550 ft Ibf/s)
inch-
inch
knot (international)
litre
pound force (Ibf avoir)
pound-mass (Ibm avoir)
              to

degree Fahrenheit
erg
foot-pound-force
pound-mass (Ibm avoir)
foot
inch-
foot-
incri
gallon (U.S. liquid)
litre
foot/minute
knot
centistoke
foot /minute
gallon (U.S. liquid)/minute
pound-force (Ibf avoir)
horsepower (550 ft Ibf/s)
metre  /second
Celsius
joule
metre-,
metre
metre&econd
metre  /second
joule  -
metre,
metre  /second
watt
metre-,
metre
metre/kecond
metre
newton
kilogram
     Multiply by

t  = (t -32)/1.8
17000 E+07
7.371 E-01
2.205 E+00
3.281 E+00
3.937 E+01
1.076 E+01
1.549 E-i-03
2.642 E+02
1.000 E+03
1.969 E+02
1.944 E+00
1.000 E+06
2.119 E+03
1.587 E+04
2.248 E-01
1.341  E-03
1.000 E-06
t  = (tp-32)/1.8
17000 E-07
3.048 E-01
9.290 E-02
5.080 E-03
4.719E-04
1.356 E+00
3.785 E-03
6.309 E-05
7.457 E+02
2.540 E-02
6.452 E-04
5.144 E-01
1.000 E-03
4.448 E+00
4.535 E-01
                                      vu

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                        ABBREVIATIONS AND SYMBOLS
ABBREVIATIONS

rn
HC
m/s
crn
kg
kg/rn
rn  /s
m
-metre
-harbor chop (confused sea) wave
-metre per second
-centimetre
-kilogram
-kilograms per metre
-square metres per second
-Newtons per metre
-cubic metres
SYMBOLS

V
*F
30
X

°c
-Critical No Oil Loss Tow Speed
-percent
-Job Order
-times

-degrees Celsius
-more than
                                     Vlil

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                                  SECTION 1

                                INTRODUCTION
      This study is a continuation of sorbent boom  testing previously carried out at
the U.S. Environmental Protection Agency's  Oil and Hazardous Materials  Simulated
Environmental Test Tank  (OHMSETT) under 3ob Order 41.  The test objectives were
performance  evaluation of the use of  a sorbent raft at the apex of a catenary oil
containment  boom and to  try to recover oil from saturated sorbent boom sections by
squeezing the boom between two rollers.  Rafts made of sorbent boom sections were
placed at the apex of conventional and sorbent oil containment booms.

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                                   SECTION 2

                   CONCLUSIONS AND RECOMMENDATIONS
      Use of  a sorbent raft  inside the  apex  of  a  catenary,  conventional oil-
containment  boom  failed  to increase the  maximum  no-oil-loss tow speed of  the
conventional boom.  Maximum no-oil-loss tow speed decreased from 0.^3 m/s to 0.33
m/s in cairn water, and from 0.^6 m/s to 0.30 m/s in the 0.3 m HC wave for the B.F.
Goodrich PFX-18 boom used.

      Increases in maximum no-oil-loss tow speeds were found using sorbent raft apex
sections.  Conventional boom sides coupled with a sorbent raft apex  section increased
no-oil-loss tow speed in calm water and 100% oil capacity from 0.25 m/s  for a  single
layer  totally sorbent boom  to  0.29  m/s for a four-layer sorbent raft apex  section.
SimUar  tests in the 0.3 m HC wave  exhibited a no-oil-loss tow speed increase from 0
m/s   to 0.22 m/s.  Oil  no longer was splashed  over the sorbent raft  at  the  apex  as
occurred  with  the  single layer  sorbent  boom.   Loss  of oil  occurred  mainly at  the
attachment points of the sorbent raft to the conventional boom sides. Vortices formed
at these attachment points, causing oil drops to be lost under the sorbent raft.

      Tests using an all sorbent  boom with a five layer sorbent raft apex again caused
increases  in no-oil-loss  tow speeds over those of a single layer sorbent boom.  Calm
water results increased from the Q-25 m/s  for  the single layer sorbent boom to 0.33
m/s, while an  increase from 0 m/s  for the single layer sorbent boom to 0.17 m/s was
found in the 0.3 m HC wave.

      Tests using apex  raft sections  varying from one to five layers showed  little
effect until  three layers were used in  the  raft.   No-oil-loss tow speed  increased 0.05
m/s for  each layer added to the apex raft for layers three, four, and five.

      Regeneration of  the  used sorbent boom  sections and  recovery  of the sorbed
fluid was  attempted using a Petro-Trap wringer with a powered roller. The Petro-Trap
wringer (Figure 1)  is designed  to squeeze oil  from  sorbent  pads.   The rollers are
smooth, and tension is provided by springs on the top roller. Saturated boom sections
       1.     McCracken, W.E.   Performance  Testing of  Selected  Inland Oil Spill
Control Equipment.  EPA-600/2-77-150,  U.S. Environmental  Protection Agency, Cin-
cinnati, Ohio, 1977.  113 pp.


       2.     Smith,   G.F.    Performance  Testing  of  Selected  Sorbent  Booms.
EPA-600/7-78-219, U.S.  Environmental Protection Agency, Cincinnati, Ohio, 1978.  35
pp.

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were  weighed  and then fed (pulled)  between the  rollers, and samples of  the  fluid
squeezed  from the boom were taken.  These attempts at boorn regeneration  were
futile; the opening between the squeeze rollers was  too  small for the boom to pass
through easily, and the smooth  rollers could not grip the oily boom sufficiently to feed
the boom  between the rollers.  Fluid-saturated boom sections contained 6 to 12 times
dry boom weight of an 85%  oil  content fluid.  It should be noted that only the medium
viscosity,  naphthenic oil was  used  in  these tests;  different oils  will yield  different
results.
   Figure 1. Regeneration of saturated boom sections using a Petro-Trap wringer.

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                                   SECTION 3

                                  MATERIALS
      The two sorbent booms tested during this program are listed in Table 1.

                 TABLE 1. SORBENT BOOM SPECIFICATIONS


Manufacturer
Boom section
dimensions
diameter length
Sorbent type (cm) (m)

Weight
(kg/m)
Sorbed oil
capacity
(multiples of
boom weight)
3M Company
3M Center 53-4
St. Paul, MN

Conwed Corporation
332 Minnesota St.
St. Paul, MN
Polypropylene    20
Vegetable fiber   20
3.0
         1.6
1.6
            13-25
15-22
      The  3M  Company  Type  270  Sorbent  Boom  (Figure  2) is  an  open-weave
polypropylene mesh bag filled with polypropylene fiber. The tension member consists
of a 0.95 crn diameter polypropylene rope connected by shackles and steel rings so that
the boom ends overlap.

      The Conwed Corporation Heavy Duty Sorbent  Boom (Figure 3) is made of a
vegetable fiber mat and a foam  floatation  strip sealed inside a polypropylene  mesh
bag.  Steel  rings and snaps  connect sections so that the ends overlap.  A 0.95  cm
polypropylene rope is the tension member.

      A straight grade naphthenic lubricating oil was used as the test fluid for this
test program. Ambient temperature during this program ranged from 20 C to 22.2 C.
Test fluid properties are shown below:
      Viscosity


      Specific Gravity

      Surface Tension
          262 centistokes @ 19.8 C
          39 centistokes @  53.3 C

          0.927

          33.5 dynes/cm

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"~"~  FTf>Cire""2T  3M Company Type 270 sorbent boorn.
Figure1 3.  Conwed Corporation heavy duty sorbent boom.




                          5

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       Inter facial Tension
       % Water and Sediment
9.37 dynes/cm with OHMSETT tank water of
ppt salinity

0.1%
      Regeneration of oil soaked boom sections was attempted by  using a Petro-Trap
wringer available  from  Petro-Trap,  Westport,  MA 02790.  The wringer is  shown in
Figure 4 and  5.
                Figure 4.  Regeneration of oil-soaked boom sections.

       Wringer unit  was welded to a barrel  top.   Holes were cut in the barrel top,
allowing the liquid squeezed from the  boom  sections to drain into  the barrel.   An
overhead, 454 kg jib crane placed  the saturated booms on a plywood table leading to
the wringer. A rope was tied  to boom section end and threaded between the rollers.
Pulling on the rope started each boom section through the rollers. A 447 kw,  12 volt
electric motor is attached  to the lower, tapered roller and was used in addition to four
people on the rope to pull each boom section through the regenerator.

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                                                     447 kw, 12V DC
                                                      Motor
                       18"
                                                         2Y*" Dia.
      2 3/4" Dia.
2 1/4" Dia.
                                                          3 3/4" Dia.
Figure 5.  Typical assembly of Petro-Trap wringer rollers.

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                                   SECTION 4-

                         EXPERIMENTAL PROCEDURES
BOOM PERFORMANCE TESTS

       Tests were  conducted without oils first, to find the upper tow speed stability
limit  for each  boom.  After  establishing the  wave conditions (if any) on the tank
surface, the boom was towed at increasing speed until the apex of the boom either
submerged  enough so that water flowed over the boom. Tow speed was increased and
decreased 0.05 m/s around the limit to reconfirm its magnitude.

       Tow tests with oil were similar to stability tests. An oil slick was placed on the
tank surface equivalent to twenty-five  percent of the  boom's maximum recommended
capacity.  Oil was pumped from storage tanks on the main bridge through a meter  to
an overflow weir distribution manifold.  The manifold is a 15 cm  pipe,  ^.6 m long with
a 2.5 cm wide longitudinal slot near the  top.  Oil fills the pipe and flows out of  the slot
onto a slash plate.  A cloth flap attached to the splash  plate allows  the  oU to flow
gently onto the water surface regardless of wave condition.  The boom was then towed
at increasing speed until failure, first in calm  water and  then  in waves.  Failure was
defined to occur when oil loss was observed under, through, or over the boom sections.
If  other modes of oil  loss such as loss between sorbent  sections at the attachment
points or at the points where  the sorbent boom attached  to the B.F.  Goodrich boom
were  observed;  they  were  noted, but not  used to  determine critical tow speed.
Additional oil was then added  to the slick to obtain 50%, 75%,  100%, and 125% of the
boom's recommended capacity.  Both cairn water and  wave tests were conducted for
each oil and load level. Photographic documentation  included 16-mm color movies and
35-mm color slides.

PHASE A

       Phase A tests determined the  effect of  placing a  raft  made of sorbent boom
sections inside  the apex  of  a  conventional oil  containment boom and  increasing tow
speed until the oil preload began to be lost.  A  raft of  ten sorbent boom sections (3.05
m  per section) was tied inside the apex  of a 63.1 m  long B.F. Goodrich PFX-18 boom
deployed in a catenary  configuration (Figure  6).

PHASE B

       A sorbent raft replaced the  conventional boom  section at  the catenary apex  in
Phase B testing.  This left four 6.09 m  long  conventional boom sections on each side.
Fourteen sorbent boom sections (^2.7 lineal metres) as shown in Figure 7 were used  to
make the raft.  Four sorbent boom rows were tied together with 10 mm polypropylene
rope.   The  first and third layer were made of four  sorbent boom sections connected
end to end and the second and fourth rows were  made of three sections.  Polypropylene

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                                      Oil Distribution  Manifold
Main Bridge
                             Bridge
                             House
                        Tow Direction
                                  Sorbent Boom Raft
                                  10 Sections 3.05 m long
           9 Sections of  B.F.  Boodrich
           18 PFX Seaboom,  6.09  m long


Auxiliary Bridge
          Figure 6. Boom configuration for Phase A testing.

                                9

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           Main Bridge
I
                                             Oil Distribution Manifold
                                   Bridge
                                   House
                                   Tow Direction
                    Four sections of B.F.  Goodrich
                    18 PFX Seaboom, 7.01 m long on
                    each side
                                    14 Sections of
                                    Sorbent Boom,
                                    3.05 m long
     Auxiliary Bridge
                 Figure 7. Boom configuration for Phase D testing.

                                      10

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rope was also used to attach the first row of the sorbent raft to the conventional boom
ends. The first row of the sorbent boom raft overlapped the down current side of the
conventional boom by 0.6 meter to minimize joint leakage.

PHASE C

      Phase C tests were performed using a 64 m long, single row, sorbent boom in a
catenary configuration.  An eighteen section sorbent boom raft was  attached to the
back of the apex as shown in Figure 8.

BOOM REGENERATION TESTS

      Upon completion of the towing  tests,  those  sections of each  sorbent  boom
judged to be most highly saturated were weighed and then pulled  through the Petro-
Trap  wringer.    The fluid  recovered  was analyzed  to determine  the percent of
recoverable oil.  The weight of the dry boom was subtracted from the  weight of the
saturated boom to determine the weight of fluid picked up.
                                     11

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                                         Oil Distribution Manifold
                36 sections of
                Sorbent  Boom,  3.05 m long
Auxiliary Bridge
          Figure 8. Boom configuration for Phase C testing
                                12

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                                   SECTION 5

                           RESULTS AND DISCUSSION
       Results  for  all tests are shown in Tables 3  through  8.   Oil  loss generally
occurred as oil droplets  entrained in the water passing under the boom in Phase A
testing and all harbor chop tests.  Calm water tests in Phases B and C exhibited oil
losses as a  surface slick.  Oil appeared on the downstream side not as droplets rising to
the surface, but as a surface slick passing under the boom sections.

       Phase A testing, utilizing sorbent rafts  in conjunction with the  B.F. Goodrich
PFX-1S containment boom, showed an overall decrease in maximum no-oil-loss tow
speed in both calm  water  and the  HC  wave when compared to results for the B.F.
Goodrich boom alone.   The sorbent raft generated oil drops when it struck the B.F.
Goodrich boom.  These drops were then swept under the sorbent raft and the B.F.
Goodrich boom.

       Phase B tests using  B.F. Goodrich containment boom sides and a sorbent raft at
the ape* exhibited increased no-oil-loss  tow speeds in calm  water, but no change in HC
waves.   Using a raft of Conwed Corporation Heavy Duty Sorbent Boom as the apex
section caused an average increase of 0.08 m/s in calm water and a 3M Company Type
270 Sorbent  Boom  raft  showed an average increase  of 0.03 m/s.  Oil loss generally
occurred at  the  points  where the sorbent  raft apex  section  was attached  to  the
conventional boom  sides.  Sorbent  boom sections  of  the raft were overlapped on  the
aft side of  the conventional boom for 3  metres, but turbulence  from currents near the
end of the  conventional boom caused oil droplets to be driven down into the water and
under the boom.

       Tests  in Phase C  using sorbent boom for the sides along with a sorbent raft at
the boom apex showed increased no-oil-loss tow speeds in calm water  and  decreased
no-oil-loss  tow speeds in the HC  wave.  Conwed  Heavy  Duty Sorbent Boom used in
Phase C effected an average increase of 0.13 m/s in calm water with the 3M Type 270
boom generating an average increase of 0.14 m/s, also in calm water.  In the 0.3-m HC
wave,  decreases of  0.05 m/s  were  found with  both booms.  Oil  was lost  by sorbent
boom sections  in the raft  section striking each other in  the harbor  chop  wave.  Oil
drops were squeezed out of the sorbent sections and driven  down into the water by  the
turbulence  caused by the waves and the  boom sections colliding.

       Tests were performed to determine the effect of changes in  the number of rows
added to the sorbent raft.  Table 2 gives the  results,obtained in Phase C testing, using
Conwed  Sorbent  Boom,  cairn water,   and 0.97 m  of oil.   No-oil-loss  tow speed
increased only after more than three rows were used to form the raft. Up to five rows
were used  to form the raft, and the fourth and  fifth rows increased the maximum no-
oil-loss tow speed by 0.05 m/s  for each row.


                                        13

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           TABLE 2.  RESULTS OF ADDED ROWS TO SORBENT RAFT
Raft rows
1
2
3
4
5
No-oil-loss tow speed (m/s)
0.20
0.10
0.20
0.25
0.30

- poorly rigged




       Regeneration of saturated  boom  sections was unsuccessfully attempted using
the Petro-Trap  wringer.  Difficulty  was encountered in forcing the boom sections
between the wringer  rollers.  No more than one metre of any boom section could be
pulled through  the wringer  rollers at a time,  and then only  with  several  people
assisting the  regenerator's  motor  to  pull the boom through  the  rollers  (Figure 1).
Samples of  the  fluid recovered by this operation  were  analyzed  for oiL and water
content.  Conwed Sorbent boom sections contained 18.3  kg/m or 2.03nru/rn of fluid
containing 84%  oil and 3M  Sorbent boom contained 11.2 kg/m or  1.2m /m of fluid
containing 85%  oil.  Due to the  small amount  of sorbent boom  squeezed, these results
cannot and should not be considered to represent the oil content or total fluid volume
of the entire sorbent boom or sorbent raft.

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TABLE 3. 3M COMPANY TYPE 270 SORBENT BOOM RESULTS

Test
no.
1A
2A
3A

4A
5A
6A
7A
8A
9A
10A
11 A
12A
Wave
Calm
0.3 m HC
Calm

0.3 m HC
Calm
0.3 m HC
Calm
0.3 m HC
Calm
0.3 m HC
Calm
0.3 m HC
Oil quantity
3 %of
m capacity
0
0
0.38

0.38
0.76
0.76
1.17
1.17
1.51
1.51
1.89
1.89
0
0
25

25
50
50
75
75
100
100
125
125
Maximum no
loss tow
speed - V Type of
m/s failure
0.89
0.89
0.48

0.41
0.43
0.41
0.36
0.43
0.30
0.30
0.33
0.30
submergence.
submergence.
droplet shed.

droplet shed.
droplet shed.
droplet shed.
droplet shed.
droplet shed.
droplet shed.
droplet shed.
droplet shed.
droplet shed.
Comments


Turbulence caused by
sorbent raft sections
causes oil to form droplets
and be swept under
boom skirt.










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TABLE it. 3M COMPANY TYPE 270 SORBENT BOOM RESULTS
.
Test
no.
IB
2B
3B
^B
5B
6B

7B
8B
9B
10B
11B
12B
Wave
Calm
0.3 m HC
Calm
0.3 m HC
Calm
0.3 m HC

Calm
0.3 m HC
Calm
0.3 m HC
Calm
0.3 m HC
Oil quantity
%of
m capacity
0
0
0.38
0.38
0.76
0.76

1.17
1.17
1.51
1.51
1.89
1.89
0
0
25
25
50
50

75
75
100
100
125
125
Maximum no
loss tow
speed - V Type of
m/s C failure
1.02
1.02
0.23
0.20
0.25
0.25

0.28
0.28
0.28
0.28
0.25
0.25
submergence.
splashover .
slick under boom.
droplet shed.
slick under boorn.
droplet shed.

slick under boom.
droplet shed.
slick under boom.
droplet shed.
slick under boom.
slick under boorn.
droplet shed.
slick under boom.
Comments
Ends of Goodrich boom
submerged




Vortices formed at
end of Goodrich boom
throwing droplets under
raft








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TABLE 5. 3M COMPANY TYPE 270 SORBENT BOOM RESULTS
"~"L '"~'-~ ' "•"" """ -' — L "' '"' """ "' " " " " '" ' -™— --~"r — -""--• --1------11 -" 	 --i«_-™-.:. •«-:..- .-• - 1 - ..- „ _"ll_. -,r ™_ ^-,-nL-lrujr™-,, --»_--,,-_-. _n JU- ---™ ,«...._-.._».-- u." J_.-T.:. .T, —,1.-™..-,--.-™ .-™ 	 _...- 1. T
Test
no.
1C
1C
3C
4C
5C
6C
7C
8C
9C
IOC
11C
12C
Wave
Calm
0.3 m HC
Calm
0.3 m HC
Calm
0.3 m HC
Calm
0.3 m HC
Calm
0.3 m HC
Calm
0.3 m HC
Oil quantity
3 %of
m capacity
0
0
0.38
0.38
0.76
0.76
1.17
1.17
1.51
1.51
1.89
1.89
0
0
25
25
50
50
75
75
100
100
125
125
Maximum no
loss tow
speed - V
m/s C
over 1.02
over 1.02
0.46
0.15
0.33
0.15
0.33
0.10
0.41
0.10
0.38
0.13
Type of
failure Comments


slick under boom.
droplet shed. Waves cause raft sections
to hit each other producing
turbulence and driving
oil droplets under boom.
slick under boom.
droplet shed.
slick under boom.
droplet shed.
slick under boom.
droplet shed.
slick under boom.
droplet shed.

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TABLE 6. CONWED SORBENT BOOM RESULTS

Test
no.
13A
14A
15A
16A
17A
ISA
19A
20 A
21A
22A
23A
24A
Wave
Calm
0.3 m HC
Calm
0.3 m HC
Calm
0.3 m HC
Calm
0.3 m HC
Calm
0.3 m HC
Calm
0.3 m HC
Oil quantity
3 %of
m capacity
—
—
0.27
0.27
0.54
0.5**
0.81
0.81
1.08
1.08
1.35
1.35
—
—
25
25
50
50
75
75
100
100
25
25
Maximum no
loss tow
speed - V Type of
m/s failure Comments
0.81
0.71
0.43
0.36
0.36
0.36
0.36
0.36
0.36
0.30
0.36
0.36
raft driven under Goodrich Boom.
raft driven under Goodrich Boom.
droplet shed.
droplet shed.
droplet shed.
droplet shed.
droplet shed.
droplet shed.
droplet shed.
droplet shed.
droplet shed.
droplet shed.

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TABLE 7. CONWED SORBENT BOOM RESULTS
- - ' - -
Test
no.
13B
14B
15B
16B
17B
18B
19B
20B
21B
22B
23B
24B
Wave
Calm
0.3 m HC
Calm
0.3 m HC
Calm
0.3 m HC
Calm
0.3 m HC
Calm
0.3 m HC
Calm
0.3 m HC
Oil quantity
3 %of
m capacity
—
—
0.38
0.38
0.76
0.76
1.1*
1.1*
1.51
1.51
1.89
1.89
—
—
25
25
50
50
75
75
100
100
125
125
Maximum no
loss tow
speed - V Type of
m/s failure Comments
0.91
0.86
0.36
0.25
0.33
0.25
0.36
0.25
0.30
0.15
0.36
0.15
ends of Goodrich Boom Submerge.
ends of Goodrich Boom Submerge.
droplet shed.
droplet shed.
droplet shed.
droplet loss
droplet shed.
droplet shed.
droplet shed.
droplet loss
droplet shed.
droplet shed.

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                            TABLE 8. CONWED SORBENT BOOM RESULTS
M
O
. - . -
Test
no.
13C
14C
15C
16C
17C
18C
19C
20C
21C

22C

23C

2*C

25C
26C
27C


28C
29C
Wave
Calm
0.3 m HC
Calm
0.3 m HC
Calm
0.3 m HC
Calm
0.3 m HC
Calm

0.3 m HC

Calm

0.3 m HC

Calm
0.3 m HC
Calm


Calm
Calm
Oil quantity
%of
m capacity
0.97
0.97
1.93
1.93
2.89
2.89
3.86

3.86

4.83

4.83

—
—
0.62


0.72
0.86
25
25
50
50
75
75
100

100

125

125

—
—
25


25
25
Maximum no
loss tow
speed - V Type of
m/s failure Comments
0.91
0.86
0.30
0.20
0.36
0.20
0.25
0.25
—

—

—

—

0.91
0.86
0.10


0.20
0.25
raft folds over. five layer raft.
raft submarines.
slick under boorn.
droplet shed.
droplet shed.
droplet shed.
slick under boom
droplet shed.
boom sections totally saturated after
20C.
boom sections totally saturated after
20C.
boom sections totally saturated after
20C.
boom sections totally saturated after
20C.
raft folds over. two layer raft.
raft submarines, two layer raft.
slick under boom, failure due to
rigging - rerigged,
layer raft.
slick under boom, three layer raft.
slick under boom, four layer raft.


test

test

test

test



poor
two




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                                 APPENDIX A

                           OHMSETT TEST FACILITY
                       Figure A-l.  OHMSETT Test Facility.
GENERAL
       The U.S. Environmental Protection Agency  is operating an Oil and  Hazardous
Materials Simulated Environmental Test Tank (OHMSETT) located in Leonardo, New
Jersey (Figure  A-l).  This facility provides an environmentally safe place to conduct
testing and development of devices and techniques for the control of oil and hazardous
material spills.

       The primary feature of  the  facility  is pile-supported,  concrete  tank with a
water  surface  203  meters long by 20 meters wide and with a water  depth of 2.4
meters.  The tank  can be filled  with fresh or salt water.  The tank is spanned by a
bridge capable of exerting a force up to  151 kilonewtons, towing floating equipment at
speeds to 3 meters/second  for at least  45 seconds.  Slower speeds yield longer test
runs.  The towing bridge is equipped to lay oil or hazardous materials on the  surface of
                                        21

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the water  several  meters ahead of the device  being  tested, so that reproducible
thicknesses and widths of the test fluids can be achieved with minimum interference
by wind.

      The  principal systems of the tank include a wave generator and beach, and a
filter  system.  The wave generator and adsorber beach have capabilities of producing
regular waves to 0.7 meter high and to 28.0 meters long,  as well as a series of 1.2
meters high reflecting,  complex waves meant to simulate the water  surface  of  a
harbor or the  sea.  The  tank water is clarified by recirculation through a 0.13 cubic
meter/second  diatomaceous earth filter system to  permit full use of a  sophisticated
underwater photography  and video imagery system, and to remove the  hydrocarbons
that enter  the tank water as a result of testing.  The  towing bridge has a built-in
skimming barrier which can move oil onto the North end of the tank for cleanup and
recycling.

      When the  tank  must be emptied for  maintenance purposes, the entire  water
volume, or  9842 cubic meters is filtered and treated until it  meets all applicable State
and Federal water  quality standards before  being discharged.  Additional  specialized
treatment may be used whenever hazardous materials are  used for tests.  One such
device is a trailer-mounted carbon treatment unit for  removing organic materials from
the water.

      Testing at the facility  is served from a 650 square meters building adjacent to
the tank.  This  building houses offices, a quality  control  laboratory (which is  very
important since  test fluids and tank water are both recycled), a small machine shop,
and an equipment preparation area.

      This government-owned,  contractor-operated  facility is available  for testing
purposes on a cost-reimbursable  basis. The operating contractor, Mason  
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TECHNICAL REPORT DATA
(Please read Instructions on the reverse before completing)
1. REPORT NO. 2.
FPA-finn/?-fii- /b>%
4. TITTTfe AND STJ8TTTLE
DEPLOYMENT CONFIGURATIONS FOR IMPROVED OIL CONTAIN! 1ENT
WITH SELECTED SORBEW BOOMS
7. AUTHOR(S)
Gary F. Smith
9. PERFORMING ORGANIZATION NAME AND ADDRESS
Mason & Hanger-Silas Mason Co., Inc.
P.O. Box 117
Leonardo, NJ 07737
12. SPONSORING AGENCY NAME AND ADDRESS
Municipal Environmental Research Laboratory - Cin., OH
Office of Research and Development
U.S. Environmental Protection Agency
Cincinnati, Ohio 45268
3. RECIPIENT'S ACCESSION»NO.
5. REPORT DATE
September 19&1
6. PERFORMING ORGANIZATION CODE
8. PERFORMING ORGANIZATION REPORT t<
10. PROGRAM ELEMENT NO.
1 BB041
11, CONTRACT/GRANT NO.
68-03-2642
13. TYPE OF REPORT AND PERIOD COVERE
Final
14. SPONSORING AGENCY CODE
EPA/600/14
15. SUPPLEMENTARY NOTES
   Project Officer:   John S.  Farlow  (201)  321-6631
16. ABSTRACT
      Performance tests  on three catenary oil  containment configurations using sorbent
 booms sections  alone and in conjuction with a conventional  containment boom,
 were conducted  at the U.S.  Environmental Protection Agency's Oil  and Hazardous
 Materials  Simulated Environmental  Test Tank (U.S.  EPA OHMSETT).   Other test variables
 included wave condition, tow speed, and oil' quantity encountered.  Maximum no-
 oil-loss containment tow speed was determined for  each wave and  oil  quantity tested.
      The use of an all-sorbent boom with a multi-layer sorbent raft at the apex
 exhibited  average increases in no-oil-loss tow speed of 0.13 m/s  over previous
 results  using a single layer boom in calm water.
      Use of a sorbent raft inside the apex of a conventional containment boom
 increased  turbulence and caused oil loss at lower  speeds than use of the conventional
 boom alone. No-oil-loss tow speeds using the sorbent boom raft at the boom apex
 also decreased  from previous results using a single layer sorbent boom in the
 0.3-m harbor chop wave.  Loss was due to increased turbulence from raft sections
 striking each other from the wave action.
      Recovery of sorbed fluid and regeneration of  the boom sections was unsuccessfully
 attempted  using a commercially available sorbent and wringer.
17. KEY WORDS AND DOCUMENT ANALYSIS
a. DESCRIPTORS
Performance Tests
Booms (equipment)
Sorbents
Water Pollution
Oils
13. DISTRIBUTION STATEMENT
Release to Public
b.lDENTIFIERS/OPEN ENDED TERMS
Spilled Oil Cleanup
Sorbent Oil Booms
Sorbent Regeneration
19. SECURITY CLASS (This Report)
UNCLASSIFIED
20. SECURITY CLASS (This page)
UNCLASSIFIED
c. COSATI Field/Group

21. NO. OF PAGES
31
i
22. PRICE
EPA Form 2220-1 (9*73)

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