United States Environmental Protection Agency Risk Reduction Engineering Laboratory Cincinnati, OH 45268 Research and Development EPA/600/S2-88/058 Jan. 1989 EPA Project Summary Granular Activated Carbon Adsorption With On-Site Infrared Furnace Reactivation Wayne E. Koffskey and Benjamin W. Lykins, Jr. The costs associated with the design, construction, operation, and mainte- nance of a 3 million gallons per day (mgd) post-treatment granular activated carbon (GAC) adsorption and reactiva- tion system were evaluated over a 2.4 yr operational period. The adsorption sys- tem consisted of three 1-mgd GAC pres- sure contactors designed with a nozzled plenum plate underdrain, each contain- ing 1,857 ft3 of granular activated car- bon. The reactivation system was com- prised of a microprocessor-controlled Shirco infrared reactivation furnace, three GAC storage tanks, and a water slurry GAC transport system. The over- all design and construction costs were $2.25 million while operation and main- tenance costs,excluding amortized capital costs, were determined to be 20 cents/lb of reactivated GAC or 14 cents/ 1,000 gal of treated water. The use-related GAC morphological changes, GAC adsorption performance, and GAC loss were evaluated for four GAC lots over 4 to 5 reactivation cycles. While some variability in GAC morphol- ogy was indicated, the GAC organics loading data, obtained for various GAC lots over successive reactivation cycles, Indicated that the adsorption performance of the reactivated GAC was equal to or greater than that of virgin GAC for all parameters monitored. The GAC loss observed during reactivation averaged 8.6% and was comprised of 7.1% reactivation loss and 1.5% trans- port loss. The effluent streams of the infrared reactivation furnace were examined for the presence of polychlorinated diben- zodioxins and polychlorinated diben- zofurans. While trace levels of some of these substances were observed, a risk assessment indicated a maximum life- time risk of three in 1 billion for the existing facility. Another objective of this research ef- fort was to obtain bacteriological infor- mation at the surface of the GAC within the adsorption system and in the efflu- ent of the adsorption system. The GAC filter effluent contained a mean hetero- trophic plate count (HPC) of 3,137 col- ony forming units (CFU)/mL, which was comprised of approximately 50% Pseudomonas and 25% gram positive bacteria. While the HPC on the GAC surface was considerably higher with a geometric mean of 3.5 x 106 CFU/mL, similar bacterial species were observed. This Project Summary was developed by EPA's Risk Reduction Engineering Laboratory, Cincinnati, OH, to announce key findings of the research project that is fully documented in a separate report of the same title (see Project Report ordering information at back). Introduction The Mississippi River along with its tribu- taries drains nearly two-thirds of the conti- nental United States and is used as a drink- ing water source by many of the cities located along its banks. The waters of the Mississippi River and its tributaries also serve as the receivers of vast quantities of industrial and municipal wastes as well as ------- agricultural run-off, resulting in the occur- rence of trace levels of synthetic organic chemicals in this drinking water source. Of equal or sometimes greater concern are those naturally occurring substances that form halogenated by-products during the disinfection process. Other water sources, besides the Missis- sippi, also contain many of these contami- nants and several drinking water utilities are potentially facing the implementation of GAG adsorption technology to meet im- pending federal and state regulations. While previous studies have demonstrated the effectiveness of GAG adsorption for reducing the concentrations of organic contaminants in drinking water, only a few of these studies have evaluated the eco- nomics of full-scale GAG adsorption with on-site reactivation. Therefore, objectives for this study were developed to fully document the use of GAG to treat a river water source. These ob- jectives consisted of the following: • To examine the use-related morpho- logical changes in GAG resulting from reactivation. • To determine the effects of several thermal reactivation cycles on GAG adsorption performance. • To perform a material balance on GAG for several thermal reactivation cycles in order to determine the vol- ume of GAG lost across the reactiva- tion furnace and in the GAG transport system. • To accumulate and evaluate cost in- formation forthe design, construction, operation, and maintenance of a full- scale GAG facility with on-site thermal reactivation. • To determine the presence and sig- nificance of polychlorinated dibenzo- dioxins and polychlorinated diben- zofurans in the effluent streams of the infrared reactivation furnace. • To obtain bacteriological information at the surface of the carbon within the GAG system and in the effluent water of the system. Three 1-mgd GAG pressure filters and a 215 Ib/hr infrared reactivation furnace were used during the operational period from March 1985 through February 1988. Mor- phological data and loading data for the various parameters of interest as well as bacteriological data were collected for vir- gin GAG through the fifth reactivation. Volu- metric GAG losses as well as operational and maintenance costs were determined for five reactivations of four GAG lots total- ing approximately 38,000 ft3 (966,000 Ib). Polychlorinated dibenzodioxins and poly- chlorinated dibenzofuran analyses were performed on the furnace effluent streams along with a risk assessment of the levels found. Treatment Plant Configuration Conventional Treatment Mississippi River raw water is pumped to the East Jefferson Parish water treatment plant where fluosilicic acid (up to 4 mg/L) is added followed by powdered activated carbon (2 mg/L) and cationic polyelectrolyte polymers (up to 8 mg/L) prior to clarification. After clarification, am monia gas is added to the process stream followed immediately by chlorine at a chlorine to ammonia ratio of 3:1 prior to sand filtration. After sand filtra- tion (2 gpm/ft2), zinc-sodiumhexameta- phosphate (1 mg/L) was added. Prior to entering the distribution system, aportion of the finished water was diverted to the GAG adsorption and reactivation facility. GAC Research Plant Conventional treatment plant finished water was pumped into one of the three 1 - mgd GAC contactors. Operation of the GAC contactors (20 min EBCT each) was sched- uled so that reactivation of exhausted car- bon could be done without interrupting GAC adsorption studies. Each of the GAC con- tactors was designed to withstand a differ- ential pressure of 60 lb/inz (psi) with water flowing upward for backwashing and 70 psi in a downward direction. Abeam supported underdrain contained 212 stainless steel filter nozzles for passage of the GAC effh ent. A slurry system was used to transport GAC. Four-inch pipe bent to a minimum radius of 2 ft was used for all transport lines except for those between the furnace quench tank and the reactivated GAC tank. These lines were constructed of 1.25-in. pipe to a radius of 1.5 ft. Thermal reactivation of exhausted GAC by the Shirco infrared reactivation system consisted of three sequential steps: drying, volatilization and pyrolysis of adsorbed organics, and reactivation with flue gas and steam. Exhausted GAC was fed through a rotary valve into the furnace feedhopper and into the furnace by a dewatering screw. From the feed chute in the furnace, GAC was drawn off by a woven wirebelt and leveled to a depth of 0.75 in. Reactivation was accomplished by glowbars placed above the belt. GAC Performance Organic Chemicals Organic chemical analyses performed during the study included: total organic carbon (TOG), total organic halide (TOX), volatile organics (VOA), capillary gas chro- matography (CGC) of solvent extractablt** with electron capture and flame ionizatio^ detection, and gas chromatography/mass spectrometry (GC/MS) of both volatile or- ganics and solvent extractables. Extensive data were collected from these analyses. Table 1. Average GAC Performance For A Reactivation Cycle Of 3 Months Parameter TOO, mg/L TOX, ng/L TOX-FP", fig/L TTHM, pg/L TTHM-FP', ng/L TFIC+, ng/L TECC*, ng/L Total Alkylbenzenes, ng/L Total Alkanes, ng/L Total Phthalates, ng/L Total PNAHs®, ng/L Total Nitrobenzenes, ng/L Total CHIsa, ng/L Influent 3.5 114 500 3.8 250 3.6 0.6 251 144 142 156 59 129 Effluent 1.2 9 128 0.4 70 1.2 0.1 89 109 78 32 13 6 Percent Removal 67 92 74 89 72 67 89 65 24 45 79 78 95 ' FP - formation potential + TFIC - total flame ionization concentration * TECC - total electron capture concentration ® PNAHs - polynudear aromatic hydrocarbons * CHIs - chlorinated hydrocarbon insecticides ------- ^Therefore, GAG performance for a react iva- n cycle of 3 mo was selected as atypical »**ample. This data as presented in Table 1 shows that GAG with a 3-mo reactivation cycle removed from 24% to 95%, by aver- age, of the groups of compounds evalu- ated. Bacteriological Bacteriological parameters monitored included heterotrophic plate count (HPC), total coliforms, and speciation of gram negative bacteria from the HPC analyses. The geometric mean HPC of the influent water to the GAG facility was 19 CFU/mL with an observed maximum of 330 CFU/mL. The geometric mean increased to 3,137 CFU/mL in the effluent of the GAC facility with an observed maximum of 1.6 x 105 CFU/mL. This level of biological activity produced a dissolved oxygen reduction of 3.9 mg/L across the GAC contactors from an average influent level of 8.6 mg/L to an average effluent level of 4.7 mg/L. Total coliforms were detected in the influ- ent to the GAC facility in 7 samples with a maximum of 5 CFU/100 mL and a non-zero average of 2 CFU/100 mL. In the GAC effluent, total coliforms were observed in 21 samples with a non-zero average of 1 CPU/ 100 mL and a maximum of 7 CFU/100 mL. -Disinfection of the GAC effluent reduced e HPC and coliforms to acceptable levels. Of the 19 CFU/mL HPC present in the influent water, about 80% were gram posi- tive bacteria occurring in 93% of the samples while Pseudomonas accounted for 7% occurring in approximately 20% of the samples. In the GAC plant effluent, the geometric mean of the HPC of 3,137 CFU/ mL was composed of approximately 49% Pseudomonas in about 95% of the samples and 25% gram positive bacteria in 84% of the samples. The level of HPC on the surface of the GAC was considerably higher than the plant effluent with a geometric mean of 3.5 x 106 CFU/mL. Essentially the same bacte- riological trend observed for the plant efflu- ent was also found on the surface of the GAC within each contactor. The number of unknown bacteria did not change signifi- cantly across the GAC beds but the number of picked colonies that did not regrow on nutrient agar increased from 3% to 13%. GAC Reactivation Morphology Analyses were performed on both spent and reactivated GAC to determine reactiva- tion quality and to measure any physical hanges in the GAC which may result from apeated reactivations. These analyses consisted of apparent density, percent ash, iodine number, sieve (effective size, uni- formity, coefficient, and mean particle di- ameter), molasses number, abrasion num- ber, volatile matter, phenol number, percent moisture, BET surface area, and pore size distribution. Generally, the reactivated carbon was comparable to virgin GAC. Some variations were observed, as shown in Table 2. These variations are suspected to have occurred from non-representative samples. From all indications, however, the origin GAC lot within each contactor can be continually recycled without any performance deterio- ration until it is eventually replaced through attrition by makeup GAC. Losses One of the most important economic fac- tors in determining the feasibility on on-site reactivation is the amount of GAC loss associated with both GAC transport and GAC reactivation. In order to accurately determine losses, each GAC contactor and storage tank had to be calibrated. After calibration, GAC volume measurements were performed on each vessel after back- washing from 5 to 10 min and draining for approximately 40 min. The contactors were backwashed at 900 gpm (8.2 gpm/ft2) while the flow rate used for the storage tanks was 300 gpm (2.7 gpm/ft2) because of their lack of backwash freeboard. Each pressurized GAC contactor had four measuring ports while each storage vessel had ten measur- ing ports. The backwash/drain/measure sequence was repeated a minimum of three times until the average of three GAC vol- ume measurements were within 0.05 ft of each other. This resulted in the GAC vol- umes being within 5.5 ft3 of one another or 0.3% of a full contactor load of 1,857 ft3. The average total loss was 8.6% with 7.1 % loss occurring during reactivation and 1.5% during GAC transport. Byproducts Each effluent stream of the reactivation furnace was sampled for polychlorinated dibenzodioxins (PCDDs) and polychlori- nated dibenzofurans (PCDFs) during reac- tivation of virgin and exhausted GAC. No PCDDs or PCDFs were detected during reactivation of virgin GAC indicating that the GAC did not produce or contain these compounds. However, during the reactiva- tion of exhausted GAC, PCDDs and PCDFs were observed in the stack gas of the reac- tivation furnace. Concentrations for each isomer detected were multiplied by their respective 2,3,7,8- tetrachlorodibenzodioxin (TCDD) toxic equivalence factor to determine 2,3,7,8- TCDD equivalent concentrations. The total average 2,3,7,8-TCDD equivalent concen- tration was 0.68 ng/dscm. At agas flow rate of approximately 200 dscm and a 7,000 hr operating year, an annual emission of 100 ug/yr resulted. The associated maximum lifetime risk for this level of emission was 3 x 10'9 (three in 1 billion). In addition to the PCDD and PCDF analy- ses, scrubber water, quench tank water, spent GAC, and reactivated GAC were also analyzed for the presence of halogenated and nonhalogenatedorganics and other by- products using liquid extraction and soxhlet extraction techniques. The organic content of the scrubber effluent water was generally lower than that of the GAC plant influent water. WhileTOC showed essentially no change from the influent water, TOX exhib- ited an average reduction of 42% from 118 ng/L to 69 ng/L. Similarly, the total amount of volatile organics measured was reduced 48% from 6.7 |ig/L to 3.2 ng/L. Pentane extractable hydrocarbons and chlorinated hydrocarbon insecticides also exhibited general reductions of 37% with TFIC re- duced from 4.2 ng/L to 2.7 ng/L and TECC reduced from 0.50 ng/L to0.31ng/L. For the quench tank effluent water, general reduc- Table 2. Reactivated GAC Morphology Over Successive Thermal Reactivations Reactivation Number Virgin Apparent Density (g/mL) Iodine Number (mg/g) Molasses Number Effective Size (mm) Uniformity Coefficient Mean Particle Diameter (mm) Abrasion Number Ash (%) BET Surface Area (rrf/g) AWWA Phenol (g/100g) Volatile Matter (%) 0.54 872 237 0.80 1.72 1.2 77.1 8.9 892 16.7 5.6 0.49 1070 303 NA- NA' 0.56 71.0 11.4 1066 22.1 5.7 0.54 897 224 0.57 1.86 1.12 74.4 10.0 777 18.5 6.8 0.57 777 220 0.69 1.66 1.11 77.0 8.7 714 15.6 NA' 0.56 864 228 0.66 1.69 1.06 76.2 9.1 1183 13.6 26.2 0.57 846 235 0.67 1.76 1.13 70.2 8.7 751 16.5 4.0 'NA - not analyzed ------- tions were observed in the organic content of the GAG plant influent water. Infrared reactivation removed 90% of the organics adsorbed on the GAG, based on chloroform soxhlet extraction residues. For the 3-mo reactivation cycles, chloroform residues were reduced from an average of 1.79 g/kg of GAG to 0.17 g/kg of GAG. The chloroform extracts were also analyzed for specific halogenated and nonhalogenated semivolatile organics. The results of these analyses, which were summarized by TFIC and TECC, indicated that there was only a small difference between spent GAG and reactivated GAG for those semivolatiles analyzed. The TFIC was reduced by an average of 27% from 0.059 g/kg to 0.043 g/ kg while the TECC was reduced by only 9% from 0.0079 g/kg to 0.0072 g/kg. Other sub- stances, such as PNAHs, were formed during the reactivation process. Costs The average operation and maintenance (O&M) GAG transport and reactivation cost was 20.4 cents/lb. The O&M GAG transport cost was 1.6 cents/lb and was comprised of 1.1 cents/lb for GAG loss, 0.3 cents/lb for operating labor, and 0.2 cents/lb for water. The cost associated with GAC loss was determined using an average transport loss of 1.5% while that for water consumption was derived from an average figure of 372,000 gal/reactivation, which included three backwashes per vessel for volume measurement. The operating labor cost for GAC transport was estimated on 12.5 hr/ reactivation and included 2.5 hr of transport time, 0.5 hr for paperwork, and 9.5 hr for drain and volume measurements per ves- sel. The O&M GAC reactivation cost was esti- mated at 18.8 cents/lb and included 5.8 cents/lb for electricity, 5.3 cents/lb for GAC loss, 3.6 cents/lb for maintenance labor, 1.7 cents/lb for maintenance material, 1.5 cents/lb for operating labor, 0.7 cents/lb for water, and 0.2 cents/lb for laboratory. The cost of electricity was based on an average usage of 46,508 kwh/reactivation deter- mined over 11 reactivations with the after- burner in operation. The cost for GAC loss was determined using an average 7.1% loss per reactivation. The cost of operating labor was estimated at 63 hr/reactivation, which included an estimated 15 min/hrfor taking readings and observing system operation over an average period of 10.5 days. The cost of maintenance labor was based on the actual maintenance hours used for the last 15 reactivations, which averaged 136 hr/reactivation. A total maintenance material cost of $16,876 incurred over 20 reactivations along with an average reacti- vated GAC volume of 1,789 ft3 was used to determine the O&M maintenance material cost for GAC reactivation. The figure of 1.7 cents/lb does not reflect any materials re- placed under warranty, the cost of the even- tual repair or replacement of the corroding duct between the furnace and the after- burner, or the cost of eventual belt replace- ment at approximately $10,000. The cost for water consumption was derived using the average water consumption over 15 reactivations of 1,280,500 gal/reactivation. The overall O&M cost for the GAC adsorp- tion and reactivation facility for a 3-mo reac- tivation cycle with a 20 min EBCT was estimated at 13.7 cents/1,000 gal. This cost was comprised of 2.8 cents/1,000 gal for GAC contactor operation, 0.9 cents/1,000 gal for GAC transport, and 10.0 cents/1,000 gal for GAC reactivation. The O&M cost for the GAC contactors was further broken down to 2.0 cents/1,000 gal for electricity, 0.6 cents/1,000 gal for operation labor, and 0.2 cents/1,000 gal for laboratory. Conclusions • Loading curves for all parameters monitored indicated that reactivated GAC adsorption performance was equal to or greater than that of virgin GAC. • While coliforms were detected in both the influent and the effluent of the GAC contactors, the levels found were not statistically different indicat- ing essentially no change in coliform density across the GAC contactors. • The overall magnitude of morphologi- cal changes observed after repeated reactivations was minimal indicating that the original GAC lot within each contactor can be continually recycled until it is eventually replaced through attrition by make-up GAC. • The average total GAC loss observed for the reactivation and transport of 20 GAC lots was 8.6%. This total GAC loss was comprised of 7.1% reactiva- tion loss across the infrared reactiva- tion furnace and 1.5% GAC transport loss. • While some polychlorinated dibenzo- dioxin and dibenzofuran isomers were observed in the infrared reacti- vation furnace stack gas equivalent to a 2,3,7,8-tetrachlorodibenzodioxin emission of 0.68 ng/dscm, the lifetime risk level assessed for this level of emission at the Jefferson Parish site was 3 X 10'9 or three in 1 billion. • No polychlorinated dibenzodioxins or dibenzofurans were found in any of the process streams of the reactiva- tion furnace during the reactivation of virgin GAC indicating that these sub- stances originated from the organic substances and chlorine species ad- sorbed onto the spent GAC as op- posed to being inherent in the infrared reactivation process. •All plumbing inside the contactors and storage vessels should be made of 316L stainless steel to prevent an eventual failure from the rapid corro- sion produced by GAC fines on car- bon steel. • The average O&M GAC transport and reactivation cost was 20.4 cents/lb. Transport cost was 1.6 cents/lb and reactivation cost was 18.8 cents/lb. Overall O&M cost for a 3-mo reactiva- tion cycle with a 20 min EBCT was 13.7 cents/1,000 gal. The full report was submitted in fulfillment of Cooperative Agreement No. CS806925 by the Jefferson Parish, Louisiana Depart- ment of Public Utilities under the sponsor- ship of the U.S. Environmental Protection Agency. ------- Wayne E. Koffskey is with the Jefferson Parish, Louisiana Department of Public Utilities, Jefferson Parish, LA 70121. Benjamin W. Lykins, Jr. is the EPA Project Officer (see below). The comphte report, entitled "Granular Activated Carbon Adsorption With On-Site Infrared Furnace Reactivation" (Order no. PB89-110 134/AS; Cost: $19.95, cost subject to change) will be available only from: National Technical Information Service 5285 Port Royal Road Springfield, VA 22161 Telephone: 703-487-4650 The EPA Project Officer can be contacted at: Risk Reduction Engineering Laboratory U.S. Environmental Protection Agency Cincinnati, OH 45268 United States Environmental Protection Agency Center for Environmental Research Information Cincinnati, OH 45268 BULK RATE POSTAGE & FEES PAID EPA PERMIT NO. G-35 Official Business Penalty for Private Use $300 EPA/600/S2-88/058 ------- |