Proceedings: Symposium on Flue Gas
Desulfurization,  Houston, October 1980.  Volume 1
Research Triangle Inst.
Research Triangle Park,  NC
Prepared for

Industrial Environmental Research Lab
Research Triangle Park,  NC
Apr 81
                     U.S. DEPARTMENT OF COMMERCE
                  National Technical Information Service
                                  NTTIS

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                                EPA-600/9-81-G19c,

                                          April 1981
Proceedings:  Symposium on
  Flue Gas Desulfurszation -
   Houston, October 1980;
               Volume  1
             Franklin A. Ayer, Compiler

             Research Triangle Institute
                 P.O. Box 12194
        Research Triangle Park, North Carolina 27709
              Contract No. 68-02-3170
                  Task No. 33
          EPA Project Officer: Julian W. Jones

        Industrial Environmental Research Laboratory
      Office of Environmental Engineering and Technology
           Research Triangle Park, IMC 27711
                  Prepared for

        U.S. ENVIRONMENTAL PROTECTION AGENCY
          Office of Research and Development
              Washington, DC 20460

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TECHNICAL REPORT DATA
(Please read Instructions on the reverse before completing)
1. REPORT NO. 2.
EPA- 600/9- 81-019a
4. TITLE AND SUBTITLE Proceedings : Symposium on Flue Gas
Desulfurization— Houston, October 1980; Volume 1
7. AUTHOR(S)
Franklin A. Ayer, Compiler
9. PERFORMING ORGANIZATION NAME AND ADDRESS
Research Triangle Institute
P.O. Box 12194
Research Triangle Park, North Carolina 27709
12. SPONSORING AGENCY NAME AND ADDRESS
EPA, Office of Research and Development
Industrial Environmental Research Laboratory
Research Triangle Park, NC 27711
3. RECIPIENT'S ACCESSION NO. ;
PB81 243156
6. REPORT DATE J
April 1981
6. PERFORMING ORGANIZATION CODE
8. PERFORMING ORGANIZATION REPORT NO. •,
10. PROGRAM ELEMENT NO.
1NE828
11. CONTRACT/GRANT NO.
68-02-3170, Task 33 j
1
13. TYPE OF REPORT AND PERIOD COVERED '
Proceedings; 10/80 \
14. SPONSORING AGENCY CODE \
EPA/600/13 }
15. SUPPLEMENTARY NOTES IERL.RTP project officer is Julian W. Jones , Mail Drop 61, *
919/541-^2489. EPA-600/7-79-167a and -167b are the proceedings of the previous
symposium on flue eas desulfurization.
is. ABSTRACT
              two-volume proceedings document presentations at EPA's Sixth Sym-
 posium on Flue Gas Desulfurization (FGD), October 28-31, 1980, in Houston, Texas.
 Presentations covered such subjects as approaches for control of acid rain, the
 Nation's energy future, economics of FGD, legislative/regulatory developments,
 FGD research/development trends , FGD system operating experience , FGD
 byproduct disposal/utilization, developments in dry FGD, and industrial boiler
 applications .
17.
KEY WORDS AND DOCUMENT ANALYSIS 1
a. DESCRIPTORS
Pollution
Flue Gases
Desulfurization
Acidification
Climatology
Energy
Economics
Legislation
Regulations
Byproducts
Waste Disposal
Boilers
13. DISTRIBUTION STATEMENT
Release to Public
b.lOENTIFIERS/OPEN ENDED TERMS
Pollution Control
Stationary Sources
Acid Rain
19. SECURITY CLASS (This Report}
Unclassified
20. SECURITY CLASS (This page}
Unclassified
c. COSATI Field/Croup
13 B 05C
21B D5D i
r07A,07D
07B,07C
04 B
14G ISA
21. NO. OF PAGES
22. PRICE '
EPA Form 2220-1 (9-73)

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                           PREFACE

 These proceedings  for the symposium on "Flue Gas Desuifurization"
 constitute the final report submitted to the Industrial Environmental
 Research  Laboratory,  U.S.  Environmental  Protection  Agency
 (IERL-EPA), Research Triangle Park, NC.  The symposium was  con-
 ducted at the Shamrock  Hilton Hotel in Houston, TX, October 28-31.
 1980.

 This symposium was designed to provide a forum for the exchange of
 information,  including recent  technological and  regulatory develop-
 ments, on the application of FGD to utility and industrial boilers.  The
 program included a Keynote Address on the approaches for control of
 acid rain, forecasts  of energy and environmental technologies  and
 economics for the 1980's, and sessions on the impact of recent legislation
 and regulations, research and development plans, utility applications,
 by-product utilization, dry scrubbing and industrial applications. Par-
 ticipants represented electric utilities, equipment and process suppliers,
 state  environmental agencies, coal and petroleum suppliers, EPA  and
 other Federal agencies.

    Michael A. Maxwell, Chief, Emissions/Effluent Technology Branch,
 Utilities and Industrial Power Division, IERL-EPA, Research Triangle
 Park, NC, was General Chairman, and     Julian W. Jones, a Senior
 Chemical Engineer in the same branch was Project Officer and  Co-
 Chairman.

    Franklin A. Ayer, Manager, Technology and Resource Management
Department,  Center  for Technology Applications, Research Triangle
Institute, Research Triangle Park, NC, was symposium coordinator  and
compiler of the proceedings

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                           TABLE OF CONTENTS
VOLUME I
Session I: OPENING SESSION ..........................................  1
  Michael A. Maxwell, Chairman

Keynote Address: Approaches for Control of Acid Rain .........................  3
  Stephen J. Gage

The Nation's Energy Future— With Focus on Synfuels ..........................  27
  Frank T. Princiotta

FGD Economics in 1980 .............................................  49
  G. G. McGlamery,* W. E. O'Brien,
  C. D. Stephenson, and J. D. Veitch

SO2 and NOX Abatement for Coal-Fired Boilers in Japan ........................  85
  Jumpei Ando

Session 2: IMPACT OF RECENT LEGISLATION/REGULATIONS ...................  111
  Walter C. Barber, Chairman

Session 3: FGD RESEARCH AND DEVELOPMENT PLANS  ......................  113
  Julian W. Jones, Chairman

Recent Trends in Utility Flue Gas Desulfurization .............................  115
  M. P. Smith, M. T. Melia,
  B. A. Laseke, Jr.,* and Norman Kaplan

The Department of Energy's Flue Gas Desulfurization
Research and Development Program  ....................................  173
  Edward C. Trexler

EPRI Research Results in FGD: 1979-1980 .................................  183
  S. M. Dalton,* C. E. Dene,
  R. G. Rhudy, and D. A. Stewart

Session 4: UTILITY APPLICATIONS ................... - ................  231
  H. William Elder, Chairman

Test Results of Adipic Acid-Enhanced Limestone
Scrubbing at the EPA Shawnee Test Facility— Third Report ..................  233
  D, A. Bwrb,ank,* S. C. Wang,
  I. ft Meftw, wrt 4- £• Wife™*
                                               .  .                          .287
  S. B. Jackson
  Presented by William L. Wells, TVA

DOWA Process Tests, Shawnee Test Facility ...............................  311
  S. B. Jackson, C. E. Dene, and D.  B. Smith
  Presented by William L. Wells, TVA

F.G.D. Experiences, Southwest Unit 1 ........ , ..........................  327
  N. Dale Hicks* and O. W. Hargrove
* Denotes speaker

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 Results of the Chiyoda Thoroughbred-121
 Prototype Evaluation  	  347
  Thomas M. Morasky,* David P. Burford,
  and 0. W. Hargrove

 Forced Oxidation of Limestone Scrubber Sludge at TVA's
 Widows Creek Unit 8 Steam Plant	      - •     3?1
  C. L. Massey,  N. D.  Moore,
  G. T. Munson, R. A. Runyan,* and W. L. Wells

 La Cygne Station Unit No.  1 Wet Scrubber
 Operating Experience	
  Richard A. Spring

 One Button Operation Start-up of the Alabama Electric
 Cooperative FGD System	  415
  Royce Hutcheson* and Carlton Johnson
 Operation and Maintenance Experience of the World's
 Largest Spray Tower S02 Scrubbers	  433
  Robert A. Hewitt* and A. Saleem

 Dual Alkali Demonstration Project Interim Report	   453
  R. P. Van Ness,* Norman Kaplan, and D. A. Watson

 Operating Experience with the FMC Double Alkali Process	  473
  Thomas H. Durkin, James A. Van Meter,*
  and L. Karl Legatski

 Status Report on the Wellman-Lord/Allied Chemical
 Flue Gas Desulfurization Plant at Northern Indiana Public
 Service Company's Dean H. Mitchell Station	  497
  E. L. Mann*  and R. C, Adams

 Magnesium FGD at TVA: Pilot and Full-Scale Designs	     543
  E. G. Marcus, T. L. Wright, and W. L. Wells
  Presented by Landon W. Fox, TVA

 VOLUME II

 Session 5: BY-PRODUCT UTILIZATION	    	559
  Jerome Rossoff, Chairman

introduction    	             ....  561
  Jerome Rossoff

Characterization and Environmental Monitoring of
Fufi-Scate Utility Waste Disposal; A Status Report	557
  Chakra J. Santhanam* and Julian W. Jones

Evaluation of Potential Impacts to the Utility Sector
for Compliance with RCRA	           . .  603
  Val E. Weaver

EPRt FGD Sludge Disposal Demonstration and Site
Monitoring Projects	  	625
  Dean M. Golden

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Potential Effects on Groundwater of Fly Ash and FGD
Waste Disposal in Lignite Surface Mine Pits In North Dakota	  657
  Gerald H.Groenewold,* John A. Cherry, Oscar E. Manz,
  Harvey A. Gullicks, David J. Hassett, and Bernd W. Rehm

Environmental Compatibility and Engineering Feasibility
for Utilization of FGD Waste in Artificial Fishing Reef Construction	  695
  P.MJ. Woodhead, J. H. Parker, and I. W. Duedall*

Government Procurement of Cement and Concrete
Containing Fly Ash	  701
  Penelope Hansen*  and John Heffelfinger

Session 6: DRY SCRUBBING  	  711
  Theodore G. Brna, Chairman

Spray Dryer FGD: Technical Review and Economic
Assessment	  713
  T. A.  Burnett, K. D. Anderson, and R. L. Torstrick
  Presented by Gerald G. McGlamery, TVA

Spray Dryer FGD Capital and Operating Cost Estimates
for a Northeastern Utility	 731
  Marvin Drabkin* and Ernest Robison

Current Status of Dry Flue Gas Desulfurization Systems	  761
  M. E. Kelly* and J. C. Dickerman

Dry SO2 Scrubbing Pilot Test Results	  777
  Nicholas J. Stevens

SO2 Removal by Dry FGD  	  801
  Edward L. Parsons, Jr.," Lloyd F. Hemenway,
  O. Teglhus Kragh, Theodore G. Brna, and Ronald L. Ostop

Dry Scrubber Demonstration Plant—Operating Results	  853
  T. B. Hurst* and G. T. Bielawski

Session 7: INDUSTRIAL APPLICATIONS	   86;
  J. David Mobley, Chairman

Applicability of FGD Systems to Industrial Boilers	   863
  James C. Dickerman

Sulfur Dioxide Emission Data for an Industrial Boiler
New Source Performance Standard ......	   887
  Charles B. Sedman

Applicability of FGD Systems to Oilfield Steam
Generators and Sodium Waste Disposal Options  	  927
  A. N.  Patkar*  and S. P. Kbthari

Performance Evaluation of an Industrial Spray Dryer
for SO2 Control	'./:.,	  943
  Theodore G. Brna,* Stephen J. Lutz, and James A. Kezerle

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 Evaluation of Emissions and Control Technology for                                     fi5
 Industrial Stoker Boilers	,*	
   Robert D. Giammar,* Russell H. Barnes,        lfs
   David R. Hopper, Paul R. Webb, and Albert E. Weljar
                                                                                  987
 Unpresented Papers	
                                                                                  989
 Flakt's Dry FGD Technology: Capabilities and Experience .      . •  •    •  •   •
   Stefan Ahman, Tom Lillestolen, and James Farrington, Jr.

 Perspectives on the Development of Dry Scrubbing—
 _,.  _      __                                                             	
 The Coyote Story	           	
   R.O.M. Grutle and D. C. Gehri

 The Riverside Station Dry Scrubbing System	
  Gary W. Gunther, James A. Meyler, and ^ndJCeisJHanser

Evaluation of Gypsum Waste Disposal by Stacking	  1031
  Thomas M. Morasky, Thomas S. Ingra,
  Lamar Larrimore and John  6.  Garlanger

Dry Activated Char Process  for Simultaneous SO2 and
NOX Removal from Flue Gases	•	  1067
  Ekkehard Richter and Karl Knoblauch

KOBELCO Flue Gas Desulfurization Process	  1081
  Kobe Steel, Ltd.

APPENDIX: Attendees  	  1099
                                       VI

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      Session I:  OPENING SESSION
       Michael A. Maxwell, Chairman
Industrial Environmental Research Laboratory
   U. S. Environmental Protection Agency
   Research Triangle Park, North Carolina

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                              KEYNOTE ADDRESS





                    Approaches for  Control of Acid Rain





                              Stephen J.  Gage





                          Assistant Administrator





                    Office of  Research  and Development





                   U.S.  Environmental Protection Agency





                            Washington,  D.C.
Preceding page blank

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     The current situation in the Persian Gulf has once again brought
 home the stark reality of the fragile balance of our industrialized
 interdependent society.  Once again we learn that our national economy
 can be  tipped up or down by events thousands of miles away from our
 shores.  National security and foreign policy deliberations must again
 focus on the question, "What are the likely impacts on our oil imports
 of a broadened war in the Mid-East?"
     We have come to the point where we must find alternatives to foreign
 oil	and we have recognized that we have our own massive coal resources -
 a wealth of "black gold" — among the greatest known reserves existing
 anywhere in the world.  We have recognized that we must move away from our
 dependence on foreign oil to greater reliance on domestic coal.  President
 Carter and the Congress have mandated this conversion to coal as part of
 our overall National  Energy Plan.  We are beginning to move from a pre-
 dominantly oil-based  energy supply structure to one emphasizing domestic
 coal,  oil  shale,  unconventional  natural  gas and heavy oil.  And we are
also encouraging  — and succeeding in —  a vigorous energy conservation
program.

    What  this  means,  of course,  is that  we are going to be mining and
burning more of the "dirtier"  fuels.   And that means there could be a
growing air pollution  problem.   Coal  mining in the U.S. is projected to
increase from the current 700  million tons annually to 1.4 billion tons
in 1990 and 1.9 billion tons  in 2000.  Conventional combustion will

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continue to be the primary method of utilizing this coal well Into
the twenty-first century -- despite the growth of a major coal-based
synthetic fuel Industry.

     The challenge we face, therefore, 1s to maintain our air quality
as the production of pollutants from burning fossil fuels rapidly
expands.  Because of the Increased use of fossil fuels and the necessary
cost of pollution abatement, there will be increasing pressure in the
future to Improve environmental control technologies, to make them more
cost-effective and — equally Important — to achieve widespread
acceptance and operational utilization of these control systems by the
utilities and industrial facilities.  This 6th FGD Symposium is testimony
to a continuing effort by both government and industry to meet these
challenges.
     The Congress has also provided impetus for the development and
application of upgraded control technologies, like FGD.  The 1977
Amendments to the Clean A1r Act underscored the importance of control
technologies through the requirement for Best Available Control Technology
1n areas where the air is clean....and the requirement for Lowest
ffefelevable Emission Rate in "non-attainment" areas where the air is
already dirty.

     The recently issued New Source Performance Standards for utility
boilers and the forthcoming development of NSPS for industrial boilers
are typical examples of recent environmental protection efforts that

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will drive the continued research and development of environmental
control technologies.
     I think 1t is likely that Federal legislative action In the
future will not significantly weaken current environmental programs.
I believe, rather, that in the face of the pressures to relax environ-
mental controls to allow more rapid expansion of our domestic fuels
utilization, the public and Congress will continue the trend toward
careful consideration of environmental impacts of future energy
development.  While we have made progress in improving air quality
throughout the country over the last decade, the struggle is far from
over.  The recent smog episode in southern California is a grim reminder
that some parts of the nation are still  threatened with severe air
pollution under poor meteorological  conditions.
     We have made great strides in developing and demonstrating highly
efficient, reliable flue gas desulfurization technologies.  While
there are Improved coal cleaning and new combustion technologies that
are in the developmental stage, and some even at the demonstration and
pilot test stages, FGD systems are currently the only viable sulfur
control  technology capable of genera] application over the next ten years,
It has  been estimated that by 1990,  electrical utilities will have
invested  between $10 and $20 billion for construction and operation of
FGD units.

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    I see from the program that Gerald McGlamery of TVA is going to
discuss the economics of FGD systems a little later this morning.
I'm sure that those of you here representing the utilities will be
especially interested in what he has to say about TVA's latest cost
studies and experience.  From our own studies in this area, we believe
that there 1s a good dollars and cents case for converting from oil
to coal — and that includes taking into consideration the use of FGD
control equipment.  Let me cite a few figures.  To produce one million
BTU's of heat, the cost of oil is $5.18, based on a price of $30 per
                       I
barrel.  To produce the same one million BTU's of heat, the cost of
coal is $1.30, based on a price of $30 per ton.  A power plant could
save five cents per kilowatt-hour by making the conversion and using
the best available scrubber, one with a 90 percent efficiency in
reducing sulfur oxide emissions.  This translates to a savings of
$14 million per year for the average size electric generating plant
being built today.

    Where less stringent scrubber controls are required, savings
could Increase.  According to conservative EPA projections for burning
high-sulfur coals, a savings of 1/5 of a cent per kilowatt-hour
would be realized by a utility that retires even a modern oil plant,
writes off the Investment, and replaces it with a new coal-fired
facility outfitted with the best scrubber available.

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     In the United States, Japan and the Federal  Republic of Germany,
operating FGD systems using wet processes, such as lime or limestone
scrubbers, continue to show improvement.  Most of these processes are
currently capable of removing well over ninety percent of the sulfur
oxides in the flue gas.  Here, in the U.S., lime  and limestone scrubbers
have been applied to coal with a wide range of sulfur content, and they
have reliably removed the sulfur oxides from burning coals with one to
four percent sulfur content.  Many of these U.S.  high sulfur coal FGD
installations have operational reliabilities of over 90 percent.  FGD
installations on low sulfur coal have operational  reliabilities of
over 95 percent	which is similar to the Japanese experience with
low sulfur coals.
     One example of a key program in nonregenerable systems is the
lime/limestone prototype test facility at TVA's Shawnee Steam Plant.
You'll  be hearing about the latest results from that operation during
tomorrow morning's session.  The results of this  particular program
are important because over 90 percent of the U.S.  coal-fired electric
generating capacity presently committed to FGD systems involves the use
of similar lime/limestone processes.  The Shawnee program has been
directed toward obtaining answers to some of industry's concerns about
long-term reliability of the process, the large quantities of waste
sludge  generated by the scrubber, and the high capital and operating

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costs Involved.  I believe major technological Improvements and cost
reductions are possible and will be realized, as we learn from programs
such as this one.

     FGD systems are now performing reliably and effectively both here
arid abroad.  As I mentioned, in Japan, during the past decade FGD systems
have been Installed on a widespread basis.  They have operated reliably
and have had outstanding success in improving the air quality.  Dr. Ando
will speak on this subject in detail, but I'd like to cite a few statistics
to demonstrate how these systems have proven themselves in Japan.  There
is no reason why they should not be just as effective here in the U.S.

     Approximately 75% of the utility power generated in Japan is fossil-
fired steam-electric.  The balance is hydroelectric and nuclear powered.
Of the fossil-fired capacity, 85% is oil-fired (most of the oil imported)
and only 3% 1s coal-fired — so you can see that their problem with foreign
oil dependency 1s much worse than ours.  But they have reduced sulfur
oxide emissions from burning both oil and coal by 50% between 1970 and 1975,
and this has been due in great part to the use of FGD systems.  They now
have ambient S02 standards that are among the most stringent in the worlc -•
about half the yearly average emission level that we allow.
     Although Japan and the U.S. have both emerged as world leaders in
developing and applying FGD systems, Japan has generally moved ahead more
rapidly, because of its more serious commitment to solving its pollution

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 problems.  As of the beginning of last year, Japanese utilities had FGD
 systems installed, under construction, and planned for about 16% of
 their fossil-fired steam generating capacity....75% of it already
 installed and operating.
     In the U.S., on the other hand, only about 3% of the total fossil-
 fired utility capacity is presently under FGD operational control.
 There are plans or systems under construction, however, for another 12%
 of the total fossil-fired capacity.  At last count, 73 FGD units were
 in operation, with 127 units in design or under construction.  When all
 of these units are operational, over 25% of the current total U.S.
 coal-fired capacity will be equipped with FGD.  Because of this growing
 use of FGD, the total amount of sulfur oxides emitted to the atmosphere
 is expected to remain constant or even decrease slightly by the year 2000

     Even though we have made great strides in controlling sulfur oxides*
we still have a long way to go to ensure that our expanded use of coal
will not degrade the quality of our environment.  EPA has been pursuing
an aggressive air emissions program to control sulfur oxides, nitrogen
oxides,  and particulates — all released from the burning of coal.  And
all  contributors to a growing problem of acid deposition, more commonly
referred to as acid rain.  I am concerned that acid rain may become one
of the most significant environmental problems of the coming decade.   It
already poses an environmental threat to our aquatic resources and
possibly to our forest and agricultural resources as well -- a threat
                                    10

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that could Intensify with  the full-scale  development  of  our  fossil  fuel
resources.  We must therefore continue  to work  toward controlling the
emission of not only sulfur dioxides, but also  nitrogen  oxides  and
partlculates, before they  get a  chance  to get out  Into the atmosphere
    create add rain problems.
     Far from being a "gentle rain from heaven,"  add  rain  can  cause
extensive ecological  damage.   In New York's  Adirondack Mountains,  for
example, an area that was once a sport fisherman's  paradise,  acid  rain
has killed all of the fish 1n half of the high-attitude lakes.   We
cannot even guess at this time the extent of the  damage in  North American
lakes, but we strongly suspect that tens of  thousands  of lakes  are
threatened, with millions of dollars in recreation  benefits and commercial
fishing at stake.  Acid rain may also be playing  a  part in  the  decline
1n forest growth observed in both the Northeastern  United States and
southern Sweden.  Experimental studies have  shown that acid rain may
damage foliage, Interfere with the germination of seeds and the rooting
of seedlings, affect the availability of nitrogen in  the soil,  decrease
soil respiration, and deplete its nutrients.  The destruction of stone
monuments and statuary throughout the world, including the  2500 year-old
Parthenon in Athens,  Greece, has been accelerated by  add rain.

     Acid rain may even indirectly present humans with a health hazard.
If drinking water reservoirs become contaminated  with  acids,  increases
                                    11

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in heavy metal concentrations may exceed public health limits.   In
New York State, for example, water from the Hinckley Reservoir  has
acidified to such an extent that when the water comes in contact with
household plumbing systems, lead from soldered joints passes into the
water.  These concentrations exceed the maximum levels recommended by
the New York State Department of Health.
     Acid rain was once thought to be primarily an S02 problem, but
we've since learned that the phenomenon is more complicated than that.
Nitrogen oxides as well as sulfur oxides can be transformed into
potent acids when they combine with water vapor molecules in the atmos-
phere.  The result is rain that may be — as we have found in some
parts of the country -- as acidic as lemon juice.   Normal rainwater has
a pH of about 5.7; newly hatched fish, which are most sensitive to low
pH, are in serious trouble in water when its pH goes below 5.0.  The
average pH of the rain east of the Mississippi today is 4.4, which is
almost 20 times as acidic as normal.

     In the United States, the rain is most acidic in the heavily
industrialized Northeast, but the most rapid increase in acid rain seems
to be occurring in the Southeast.  This parallels  the expansion of South-
eastern urban and industrial activities that result in sulfur and nitrogen
emissions.   Here, the trend is more apparent than  in the Northeast,
because the atmosphere is more rapidly deteriorating, and fewer acidic
ions are required to cause a pH change.  Most of the West has thus far
                                    12

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escaped the add rain scourge* but Colorado,  the Los Angeles Basin,  the
San Francisco Bay Area, Spokane, Tucson, and  Portland are known exceptions.
In much of the West, the alkaline nature of the soils and lakes acts to
neutralize add rain, so the effects may not  be as pronounced there.  But
even 1n the West, ominous signs of vegetation damage have appeared.

     The Adirondack fish disaster, which occurred in an area of thin soils
and fragile, closely watched ecologies, may be only a dramatic early
warning of the damage that acid rain may someday cause on a much larger
scale.  Were 1t not for the buffering ability of the soil in other sections
of the East Coast, the rains of the 1970's could have killed off most of
the region's freshwater fish.
     Clearly, we are not talking about something that sprang from the
overactive imagination of a zealous environmentalist.  Acid rain is  a
phenomenon that demands careful attention.
     What can be done to prevent the rains of the 1980's from becoming
increasingly more destructive?  The most urgent task that EPA faces  is
to get to the bottom of what causes acid rain.  Until the perplexing
mechanisms by which acid rain is formed are better understood, attempts
to control it may miss the mark, resulting in a less than optimum use of
costly investments for control.

     It 1_s_ known that, after sulfur and nitrogen oxides are discharged
Into the atmosphere, they are oxidized into sulfates and nitrates, which
then react with moisturp in the air to become acids.  There are several
                                     13

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complicated pathways or mechanisms by which this oxidation can occur-
Which path is actually taken depends on a number of factors,  including
the concentration of heavy metals, the intensity of sunlight,  the
temperature, the humidity, the amount of ammonia present,  and  the
particulate and photochemical smog levels.
     In the eastern United States, sulfuric acid is the  major  component
of acid rain, comprising as much as 65 to 70% of the rain's acidity,
while nitric acid supplies only 25 to 30 percent.   In the  West, the
acids in acid rain are generally half nitric acid  and half sulfuric
acid, although in some western urban areas, as  much as 80% of  a rain's
acidity can be comprised of nitric acid.  Other acids can  also contribute
to the acid rain problem.  Hydrochloric acid, for  example, may be emitted
directly from coal-fired power plants and is frequently  found  relatively
short distances downwind from such sources.
     Acids may be deposited on earth not only by rain or snow, but also
through an atmospheric process called "dry deposition."   This  is the
process by which particles such as fly ash, as  well es 862 and NOX, are
deposited onto surfaces.  While these particles or gases are  normally
not in the acidic state before deposition,  it is believed that they are
converted into acids after contacting water in  the form  of rain, dew, fog,
or mist after deposition.  The precise mechanisms  by which dry deposition
takes place, and its effects on soils, forests, crops, and buildings, are
not adequately understood.  Much research is being initiated  to clarify
                                     14

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the contribution of dry deposition to the overall  add deposition
problem.

     Another aspect of add rain that demands further study,  and which
makes regulation of add rain a particularly tricky undertakinq, is
long-range transport.   This phenomenon was first recognized in  the
early 1970's.  At that time, studies on the adverse effects of  S02 and
sulfates on human health led to a stringent ambient air quality
standard for S02 as well as technological control  of S02 emissions.
The associated control efforts forced the utilization of low  sulfur
fossil fuels and scrubbers, and resulted 1n lower sulfur dioxide emissions.
Unexpectedly, however, reductions 1n urban S02 levels did not result in
proportional decreases in urban sulfates.
     Several theories were offered to explain this development.   One
explanation, the transformation-transport theory, was that reductions in
urban S02 emissions were offset by increases in rural S02 emissions  from
new power plants located outside cities.  S02 emissions from  these power
plants, the theory held, had been transformed into sulfates and transported
over long distances to urban areas.
     A project that was recently completed by EPA's Office of Research
and Development on sulfur transformation and transport seems  to bear this
theory out.  It found that sulfate aerosols could be transported hundreds
of kilometers from the initial S02 source.  This validation of  the trans-
formation-transport theory reinforces evidence indicating that  the
                                    15

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acidity of lakes in New York's Adirondack Mountains, for example, may
be caused by adds carried by winds from power plants as far away as
the Midwest.
     Under certain conditions, it appears that sulfate and nitrate
compounds can stay aloft long enough to cross continents* oceans, and
international boundaries.  This creates a situation in which the acid
rain in one country is caused by the emissions of another, but the
recipient of this damaging rain receives little or no benefit from the
source initiating the pollution.   In a few short days, local problems
can become international 1n scope.   This aspect of acid rain has caused
us problems with our northern neighbor; Canada receives two to four
times the amount of SOX that the U.S. gets from Canada, and the NOX
exchange 1s 11 times greater from the United States to Canada.  Recent
negotiations between the two countries have been aimed at confronting
this problem.  These talks are expected to evolve into a bilateral
transboundary air pollution agreement.  And, through agencies like the
United Nations Economic Commission  for Europe, the acid rain issue
vis-a-vis other countries may also  be faced.

     EPA is not alone in its  efforts to uncover the causes of and the
solutions to the acid rain dilemma.   Many government agencies as well as
private industry are participating  in these efforts.  In recognition of
the seriousness  of  the  acid rain  threat,  the President, in his Second
Environmental  Message,  called  for,a  minimum of $10 million per year to
                                    16

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be spent over the next ten  years  on  a  comprehensive  add  rain  research
program.  He also established an  Acid  Rain  Coordinating Committee
consisting of seven Federal agencies to plan  and  coordinate  a  Federal
Interagency program.   The Committee  Is co-chaired by representatives
from the Department of Agriculture and EPA, and more recently* the
National Oceanic and Atmospheric  Administration.   As one  of  the co-
chairmen of the Federal Committee, I am pleased to note that the
federal agencies are now spending over $15  million for acid  rain
research under the AEGIS of a cooperative research plan.

     In addition to generating Information  on add rain that can be
used to develop air quality control  strategies and options,  EPA has
another fundamental task:  to qommunicate to  Congress and the  public
the effects of add rain, with particular attention  paid  to  the ecologic
and economic consequences of continued high levels of add precipitation.
     One tool to accomplish this  communications function  will  be the
development of an "add deposition document," which  David Hawkins, EPA's
Assistant Administrator for A1r,  Noise and  Radiation, and I  are mapping
out.  This document will be an attempt to quantify and quality, in a
preliminary way, the entire range of pollutants involved  in  acid rain
creation — sulfur, partlculates, nitrogen  oxides, hydrochloric acid,
hydrocarbons and heavy metals.

     The document will not be a "criteria document"  in the sense that
1t will be used to develop ambient air .standards; rather, It will  put
                                    17

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the scientific evidence on add rain before the public so that It can be
discussed 1n an open forum, as well  as serve as a focal point for future
add rain research.  This document,  we hope, will be an Important step
toward fostering public debate about how we as a country will meet the
add rain challenge.
     We do know, at this time, that  some of the methods currently being
used to minimize the local effects of S02 and NOX around large sources
are actually aggravating the acid rain problem.  One method long favored
by power companies is the use of tall  emission stacks.  The rationale
behind tall stacks is that the emitted sulfur dioxide will  be carried
away from the local community by winds.   Unfortunately, the tall stacks
also keep the sulfur dioxide airborne  longer, thus making sulfate
formation more likely.

     As the mist that conceals the secrets  of acid rain formation and
transport is gradually  lifted, we will  know better what control  methods
will actually stop acid rain at its  source, rather than passing  the
problem on to someone else.   At present,  however, it appears that the
only practical  approach lies 1n reducing  SOX and NOX emissions.   Many
innovative schemes have been suggested.   There are studies  underway to
estimate the costs of various  ways to  reduce emissions of these  pollutants
and to compare  these costs  against acid  rain damage costs,  which are
only now beginning to be  understood.
                                    18

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     For SOX control, FGD will  probably remain our chief weapon through
at least 1985.  As you will  hear throughout this conference, this
technology can be applied to a  variety of sources without imposing an
unreasonable financial burden.   The use of low-sulfur coal  is another
piece of the arsenal in the  war against SOX emissions, along with the
array of technologies, both  under development and on the commercial
market, designed to remove sulfur from fuel before it is burned.  These
technologies include coal cleaning, coal gasification, and  desulfurization
of liquid fuels.  Then, there are also the combustion modification methods
that allow removal of sulfur during burning, such as fluidized-bed
combustion.

     But, as we have seen, SOX  constitutes only a piece of  the acid rain
puzzle.  NOX emissions can play an equally large role.  And while we
have found ways to hold the lid on SOX emissions, we've only recently
begun to get a handle on NOX control.  In fact, as coal use rises, we
expect that NOX emissions could increase by thirty to forty percent by
the year 2000, unless more effective control methods are developed and
quickly put to work by industry.  At present, half the current NOX
emissions come from stationary  sources; but by 2000, due to the trend
toward greater combustion of coal, stationary sources may be responsible
for up to 75 percent.  Of the emissions from stationary sources, over
half are contributed by utility and large industrial boilers alone.
These large boilers now.emit an estimated 6 million tons of NOX every
year.
                                    19

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     The solutions that are so effective for SOX control  aren't much
help when it comes to NOX control.   Physical  coal  cleaning, which can
be used on some coal  to reduce sulfur and ash content,  has no effect on
coal's nitrogen content, because the nitrogen is chemically bound to
the coal.  "Denitrogenation" — that is, chemically removing nitrogen
from coal — is prohibitively expensive at present, and at any rate does
not address the problem of thermal  NOX, which is formed by molecular
reaction in super-heated combustion air.  Flue gas treatment for NOX
control has been used with a fair amount of success in  Japan on oil-
fired boilers, but there are major financial  and technical  hurdles to
applying that technology to coal-fired units.   Even the coming age of
synthetic liquid fuels made from coal, which  may consume  120 million tons
of coal in 1990 and 300 million tons in 2000, offers little hope for NOX
control — in fact, the concentration of fuel  nitrogen  may be increased
when coal is converted to a liquid.

     However, there is a promising answer that is  both  cost-effective and
energy-efficient.  By modifying the conditions under which combustion
takes place, an existing coal-fired power plant can reduce its NOX emissions
by 40 to 50 percent.   When applied to new burner designs,  combustion
modification may reduce NOX emissions by another two-thirds, yielding a
total NOX control of up to 85 percent.  And,  because combustion modifica-
tion involves changes only in burner design,  the cost is  quite small —
less than one-h&lf of one percent of the boiler cost.   Further, because
                                    20

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we are ensuring that the new burners are as efficient as the older designs,
the operating cost 1s nearly zero.  EPA 1s aggressively developing low-NOx
burner designs.

     Ideally, one technology would simultaneously control both of acid
rain's major components.  This, in fact, is the idea behind a particularly
exciting new control technology, which may be retrofitted to many existing
coal-fired boilers with only minor modifications:  the limestone injection/
multi-stage burner, or LIMB for short.  The LIMB may be able to remove
50 to 70 percent of sulfur oxides at the same time that it reduces NOX by
50 to 80 percent.  And 1t can accomplish this at a cost for $03 control
equipment of only $30 to $40 per kilowatt, as opposed to the average of
$150 per kilowatt that wet scrubbing requires.
     Although the LIMB has only reached the bench/pilot scale stage of
development here 1n the U.S., Germany 1s currently operating a 60 megawatt
electric boiler using the technology, so we know that it works on a
larger scale.
     The Idea of combining limestone injection for $03 control with a
low NOX burner 1s not a new one.  In 1967, UOP, building on earlier
limestone Injection experiments by Combustion Engineering, injected
limestone Into an arch-fired burner, which is a naturally low NOX burner.
    emissions were reduced by 50 percent at a stoichiometric ratio of 1:3.
     The 60 megawatt prototype limestone injection, boiler in Germany,
which I mentioned earlier, has been operating for one year.  It fires
                           v'
West German lignite, and utilizes flue gas recirculation to minimize
                                     21

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peak temperature and NOX formation.   At present, 1t is achieving 50 to
90 percent S02 removal  at stoichiometric ratios of 2.5 to 5.0.  Retrofit
capital costs for this  technology are only $3.00 per kilowatt.
     EPA has proposed a five-year research, development, and demonstration
program that will bring the LIMB technology up to commercial scale.  In
the first year, EPA will characterize reactions and furnace conditions;
evaluate impacts on furnace operation; and test the technology with a
wide range of coal types and calcium-based sorbents.  Next will come a
year of field evaluation, in which EPA goals will be to demonstrate
sulfur removal efficiency, optimize performance variables* determine if
there are any adverse boiler side effects such as slagging, plugging and
corrosion, and obtain design and cost data.  Both wall-fired and tangentially-
fired units will undergo testing.  Another year will be spent installing
the LIMB technology on full-sized boilers, which will then be subjected
to two years of performance optimization and long-term evaluation.  The
development effort will be co-sponsored by EPA and the Department of Energy.
The total tab for the LIMB program will amount to $16.5 million, which
will be a bargain if LIMB fulfills its initial promise.

     Industry as well as government must play a crucial role in the
development of methods to control acid rain.  EPA has the resources to
provide the fundamental research and the testing of new control technologies,
but we must rely on industry to provide the host sites that allow tech-
nologies to be tested under real-life conditions.  And, we must depend
                                     22

-------
heavily upon the commercial expertise and engineering experience of
boiler manufacturers if a technology is to progress beyond the demon-
stration stage.

     Now there's always an element of risk for the private sector
when it invests in new equipment and new technologies.  Control processes
that look promising on the drawing board or durinq small-scale experiments
don't always pan out when they are put into practical use.  But we at
EPA truly believe that with the kind of cooperation between government
and industry we have enjoyed up to now, and with continued joint effort,
we can solve the acid rain control challenges we face.

     With a better understanding of what causes acid rain and with the
necessary control technology under development, we will be able to
begin making strides in the regulatory arena....to pull in the "reins,"
if you will forgive me, on acid rain.  As the Clean Air Act stands now,
there are no regulatory requirements concerning acid rain per sj&.  As
most of you are aware, this Act comes up for revision next year, and EPA
is consulting with other Federal agencies on the possibility of changes
that would better address the acid rain issue.

     The Clean Air Act is currently structured around a presumption
that air pollution can be related to a particular source or a well-defined
group of sources.  But, in the case of acid rain, there is no clear-cut
relationship between specific emissions and the acid rain.  In other
even though the types of emissions that lead to acid rain are known, it
                                    23

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 1s currently not possible to accurately trace individual  emissions that
 cause acid rain back to their origins.   And,  while the Clean Air Act
 has been amended to address the problem of interstate pollution, any
 given state is only able to enforce its emission limitations against
 sources within its own boundaries.   A state can petition  the EPA
 Administrator if it feels that another state  is preventing it from
 attaining a national standard or otherwise causing a deterioration in
 that state's air quality, but then  EPA is  faced with the  problem of
 how to demonstrate that one or several  out-of-state sources are
 responsible for impermissible air quality  violations.   Such a demon-
 stration would be hard, if not impossible, to make, especially if a
 number of sources from several states or nations were involved.

     One regulatory option that EPA is  reviewing is the development
 of national ambient air quality standards  for nitrates or sulfates,
 two precursors of acid rain.  However,  it  Is  not clear whether there
 is sufficient data on which to base such a standard.  Even if the
 data were available, the standard-setting  process is a lengthy one.
 It would probably be five to ten years  before any emission reduction
could be achieved.   Other near-term options include:  better monitoring
of S02 emissions to improve enforcement of existing standards; the
establishment of federal regulatory requirements for review of interstate
Impacts  of State Implementation Plan provisions; or the establishment
of new source performance standards for pollutants for which EPA has
not set  ambient standards, such as  total sulfur.
                                    24

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     A longer term option might Involve the Conaress  setting
regional  SOg and NOX emission reduction goals  — say  5 to 10 percent
per year — goals which would be administered  on a multi-state basis
and would allow the utilities and Industries to meet  the  goals on a
system-wide basis using the most cost-effective combination of
approaches — coal washing, combustion modification,  load shifting
to cleaner plants, fuel shifting, and early plant retirements, to
name a few.
     Whatever path we choose, however, we must be mindful  of the
need to consider the regulatory burden imposed on the utility or
Industry and the ratepayer or consumer.  In addition, we  must fully
support the national energy policy of expanded coal use,  and be
sensitive to the fact that the economy cannot  regain  its  vital growth
without the atd of a vigorous industrial  base.  These are "mighty
tall" orders, as they say, for the Government  and the industrial sector.
But then few people really believe that anything worth doing in this
country is going to be easy.  Why should reconciling  environmental ar.c
energy goals, a priori, be any easier than, say, reconcilings energy
goals and national security, or inflation and,unemployment objectives.
There are no easy answers, only a nation of differing but robust people
trying to work out their future.
                                  25

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            THE NATION'S ENERGY FUTURE - WITH FOCUS ON SYNFUELS
                            Frank T. Princiotta
                    Director, Energy Processes Division
               United States Environmental Protection Agency
                             Washington, D. C.
                                 ABSTRACT

     Projections indicate that coal, nuclear energy and oil shale wil"i
     become increasingly important as we adjust for static domestic oil
     and gas production and minimization oil importation.  Environmental
     problems can be quite severe for each of these fuel cycles.  A massive
     synthetic fuel industry based on coal, oil shale and biomass, is
     emerging with monumental potential for environmental damage.  The
     Environmental Protection Agency (EPA) has designed a regulatory program
     aimed at mitigating environmental damage while allowing for birth and
     nurturing of this critical industry.
Preceding page blank
                                      27

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               THE NATION'S ENERGY FUTURE - WITH FOCUS ON SYNFUELS
OUR ENERGY FUTURE

     America is making progress in minimizing  dependence of imported oil.
During the first five months of 1980,  gasoline consumption decreased 8.1
percent — compared with the same period last  year - and crude oil imports
decreased to 7.8 million barrels per day — the lowest level in four years.
Petroleum stockpiles are at capacity levels nationwide due to a very real,
conscientious effort to conserve energy in all areas:   electricity, home
heat and transportation fuel.

     Of even greater significance is passage of the Energy Security Act,
signed by President Carter in June of 1980. This  bill will promote conser-
vation, increase production of coal and oil, and help  harness the power of
the sun, wind and rivers and most importantly  spawn a  major synthetic fuel
industry based on coal, oil shale and biomass.   All of these measures can
serve as effective remedies against further reliance on costly and uncertain
supplies of foreign oil.

     To achieve the necessary growth in domestic energy resource development
to meet our future production goals, a substantial increase in extraction,
processing, transport and use of domestic fossil fuels must take place.  EPA
has recently made projections attempting to predict our nation's energy future
using the Strategic Environmental Assessment System (SEAS)  model and an EPA
sponsored study projected synfuel production.   These projections suggest that
coal, oil shale and nuclear energy will allow  for  the  nation's economic growth
despite the leveling off of domestic petroleum and natural gas and without
increasing oil imports (Figure 1-4).  For example, the amount of coal mined
in this country must expand from the current 700 million tons annually to
1.1 billion tons in 1990 to 1.6 billion tons in 2000.   The production of
synthetic liquid fuel and gas from coal is expected to consume 80 million
tons by 1990 and 350 million tons in 2000.  We can also expect that the 1980's
will see the oil shale industry emerge as a significant supplier of fuel,
producing up to 300,000 barrels per day by 1990 and 2.2 million barrels per
day by 2000.

     Such projections indicate a trend away from traditional and less environ-
mentally damaging energy sources, toward potentially more damaging fossil fuel
sources such as coal (particularly from western surface mines), oil or gas
from the Outer Continental Shelf, and western  oil  shale.  The trend also
points to the increasing use of nuclear energy to  generate electricity and
indicates an increasing interest and use of solar  and  geothermal energy.

     These major shifts toward increased use of less clean fuels can pose a
significant threat to human health and the environment.  Potential negative
impacts are likely to result from the extraction,  processing and utilization
phases of each major fuel (Figure 5).   For example, increases in coal and oil
shale mining can create erosion and subsequent surface water siltation problem?
                                      28

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    domestic fossil energy
    resource requirements
         40-
ro
CJ
"o
W


cr
                                             W = western mining
                                            ES = eastern strip mining
                                            EU = eastern underground
                                            OF = offshore—lower 48 states
                                            OS = onshore—lower 48 states
                                             A = alaskan
                                                    NOTE: Projected Oil Imports


                                                        1975: 17 QUADS
                                                        1990: 14 QUADS
                                                        2000: 10 QUADS
                                                   17.8
                1975/1990/POOO
                       1975/1990/2000
                           oil
1975/1990/2000
   gas
1975/1990/2000
  oil

-------
           FIGURE 2
          U. S. non-fossil energy
          resource requirements
CO
o
          >.
          ®
          (Q
          3
          cr
                   1.8
                        10.7
                           I
                   1975/1990/2000
                     uranium
                                  3.2 3.2
                                                S = solar
                                                G = geothermal
                                                B = biomass
              1.5
                                             S
         B
        IWM1II f%

         S
1975/1990/2000
hydroelectric
1975/1990/2000
   other

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  components of
  domestic coal
    25
    20-
o>
o>
(0
TJ
nj
3-
cr
10 —
     0
                  20.6
              16.3
            9.1
                   CM
                CM
             CM
             1975/1990/2000
               electric
               utilities
                            CK
                            4.6 5.7
                              4.7
                              CK
                              CM
                               CK
                                               CM = combustion
                                               CK = coking
                                               LI = liquefaction
                                               GA = gasification
                                                   8.0
                                     -|-jCM
                                            LI
                                            1.7
                                          0
                                                    LI
  GA
                          1975/1990/2000
                           industrial
1975/1990/2000
 conversion

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 FIGURE k
alternative fuels
production: 1985/1990/2000
thousands
of bpdoe
1200-
1000 -
 800 -
600 H
200 -
           high
            low
       1985/1990/2000

       high BTU gas
                        high
                        low
                                    high
                                    Tow
                                  high
                                  low
                                                high
                                                            high
                                                            • low
1985/1990/2000

low/medium*
 BTU gas
1995/1990/2000

  Indirect
1985/1990/2000

 direct
1985/1990/2000

  oil from
  oil shale
1985/1990/2000

  oil from
  tar sands
                                                                                 1985/1990/2000
                                                                            5,060 I
                                                                            hlghf
                                                                                                2,965}
                                                                                                 low
                                                                                               low
                                                                                             1985/1990/2000
           from coal gasification
                                                elhanol from   total production
                                                 blomass &
                                               Industrial wastes
             liquids from coal liquefaction


                           Source: Hauler, Ballly & Company Alternative Fuels Monitors: Coal Gasification and Indirect UquefaclHtn: Oil from Shale.

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lifted  U.S. domestic fuel flow: 199O
PRIMARY FUELS
EXTRACTION
c" ' '
CONVERSION/
TREATMENT
PROCESS
SECONDARY FUELS
UTILITY
ELECTRIC POWER
TRANSMISSION/
TRANSPORT
UTILIZATION DEVICES
                                 NUCLEAR
                                 POWER
                                 PLANTS
ELECTRICAL
 DEVICES
                                            ELECTRICAL
                                            POWER LINES
                 DIVERTED TO
                PETROCHEMICAL
              ?rv  INDUSTRY
               ^
                                COAL POWER
                                 PLANTS
                                                         LIQUID/GASEOUS
                                                           DEVICES
     ®®®J7Ffift
                                                   WATER  I IK? LAHD
                                                        &•

-------
groundwater quantity and quality are also likely to be affected.  Processing
coal and oil shale to synthetic liquids and gases may yield toxic emissions
and large quantities of solid wastes; and despite current regulations, an
increase in coal combustion will result in increased production of nitrogen
oxides, sulfur oxides and solid wastes (Figure 6).  The environmental and
safety uncertainties surrounding the use of nuclear energy have been well
publicized.

     Many of the adverse impacts on health and environmental quality, however,
can be controlled or avoided:  Most mined land can be reclaimed; particulate
matter and the oxides of nitrogen and sulfur can be scrubbed from flue gas;
acid precipitation and its effects on agricultural and forest production can
be reduced.

     EPA has an impressive array of legislative tools available to control
air, water and land pollution from energy and industrial sources (Table 1).
The agency will face the monumental challenge of utilizing these mandates
to achieve maximum benefit of minimum cost.

     Controlling these pollutants increases the monetary costs of energy, but
failure to control them lowers the productivity of our natural resources,
degrades the quality of our environment,  and imperils the health of our
'population.


Focus on Synthetic Fuels

     As the projections suggest our energy future should be characterized
by a massive synthetic fuel industry by the year 2000.  Although oil shale
plants will be limited to a relatively limited area (Figure 7)  coal gasifi-
cation and liquefaction plants could be constructed anywhere large quantities
of coal are located (Figure 8).  Ethanol  plants will be initially sited in
corn and wheat farming areas (Figure 9) but could eventually proliferate as
other crops and agricultural wastes become feasible as feedstocks (Figure 10).

     oo Synfuel Environmental Issues

              Synthetic fuels processes are receiving our most serious
         attention because synfuel development activity is clearly
         intensifying, because of our concern over the unknown nature
         of the pollutants which may be generated, and because of EPA's
         recognition that the enormous capital outlays involved in
         building these facilities during the next decade dictates the
         earliest possible and most stable possible environmental
         regulations for this new industry.  It is expected that
         pollutants coming from coal conversion and shale oil production
         will  be more diverse in composition than those produced by
         direct fossil fuel combustion.   The burning of fossil fuels
         in conventional processes involves complete oxidation (or
         attempts threat)  whereas synthetic fuels are produced under
                                      34

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           FIGURE  6
            growth In emissions/wastes
            from stationary sources
to
               millions
           3001 of tons
           250'
           200 i
           150
            50
                                                 net emissions (after treatment)
                 1975  1990   2000
                •TOTAL SUSPENDED
                  PARTICULARS
1975   1990  2000
*SULFUR OXIDES
1975   1990  2000
  •NITROGEN
   OXIDES
1975  1990   2000
UTILITY COAL ASH/
   SLUDGES
1975   1990  2000
  O!L SHALE
  WASTES
               "energy

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                                              TABLE  1
            AIR, WATER AND SOLID WASTE ENVIRONMENTAL
               LAWS IMPACTING FOSSIL ENERGY FACILITIES
  RELEVANT AUTHORITY
 IMPACT
  Clean Air Act Amendments of 1977
  • Set New Source Performance Standards
  (NSPS) for energy industries (Section 111).
  • Set National Emission Standards for Hazard-
  ous Air Pollutants (NESHAP) for selected
  industries (Section 112).

  • Implement Prevention of Significant Deteri-
  oration (PSD) Program (Section 160).
  • Achieve Ambient Air Quality Standards (Sec-
  tion 109).
  • Set Lowest Achievable Emission Rates
 (LAER) (Section 171).
  * NSPS set for fossil utility boilers; industrial
 boiler NSPS being developed; oii shale, coal
 gasification, and liquefaction in planning stage.

 • NESHAP requirements for synthetic fuels
 industry being evaluated as process plans become
 firm.
              *
 • PSD permits required for all New Sources
 (coal-fired boilers and synthetic fuels plants) to
 prevent increases in paniculate and SO, levels in
 areas having good air quality.

 • Require utilization of appropriate control
 technology to reduce emissions to levels required
 to meet State Implementation Plan (SIP) goals.

 « Require level of pollution control technology
 greater than that which would normally be
 required by SIP for plant siting in non-attaiment
 areas.
 Federal Water Pollution Control Act Amendments of 1977
  • Set discharge limits based on best conventional
 technology for energy industries (Section 306).
 • Set discharge limits based on best available
 technology for toxic pollutants (Section 307).
 •  Issue and enforce discharge permits to achieve
 above limits and to meet water quality standards
 (Section 402).
 • Effluent guidelines for steam-electric industry
 issued, industrial boilers must meet guidelines for
 specific industry; effluent guidelines being planned
 for oil shale and coal gasification and liquefac-
 tion facilities.

 • For designated toxic pollutants best available
 control technology will be required, and will have
 greatest impact on the design of synfuel plants.

 • Permits for electric utility plants and other
 industries being issued based or, effluent guide-
 lines, permits for synthetic fuels plants will be
 issued on basis of besi information available until
 guidelines are issued.
 Safe Drinking Water Acl of 1974

 • Review projects for possible danger to under-
 ground drinking water supplies (Section 1424).
 • All projects receiving federal assistance will be
 reviewed for processes impact on groundwater
 quality as it may impact drinking water.
 Resource Conservation and Recovery Act of 1976

 • Set criteria for defining hazardous waste
 (Section 3001).

 • Define accepiable disposal practices for
 hazardous wastes (section 3008).                 '
• Set guidelines for non-hazardous waste
disposal (Section 4004).
• Proposed procedures for determining if wastes
are hazardous have been issued.

e Utility wastes and spent oil shale classified as
"special" wastes; if hazardous, they must meet
monitoring requirements but not disposal
requirements; best economically attainable
disposable technology will be defined.

a Disposaj guidelines for non-hazardous utility
waste will be completed in 1981, other energy
wastes subject to state guidelines.
                                             36

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  FIGURE 7
 some oil shale development sites
OJ
     oil shale deposits of the Green River formation
     p!anr:fcd wod potential oil sha!e projects
                                         Wyoming
                                              SOURCE: Office •
                                                      cyy Asses;;r.-?ni

-------
     FIGURE 8
to
CD
    sites for coal-derived
    alternative fuels plants
          potential for coat-derived alternative
          fuels development

          high potential for coal-derived alternative
          fue*& development
SOURCE: U.S. Bu'oao of. Mines

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 FIGURE 9
potential sites for large-scale
ethanol production by 1985
co
uo
    [JUJ corn


    fcd~! wheat
                                          SOURCF. Hagler, Bailiy R C-oi.ipany based on information from O-
                                          of Technology Assessment, U.S Department of Energy. US Depi'

                                          of AgrlcuHure

-------
 FIGURE 10
potential sites for large-scale
ethanol production by 2000
   sweet sorghum
   agricultural & food wastes
   corn & agricultural & food wastes
   sorghum & agricultural & foc:d wastes
   com & sorghum & agricultural & food wast
SOURCE: Hagler, Bailly & Company, bdsed on Information horn Office
of Technology Assessment, U.S. Department of Energy. U.S. Department
of Agriculture

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reducing conditions using less air than is required for complete
combustion.  The result is that a wide variety of high molecular
weight organics, reduced sulfur compounds, and other potentially
toxic compounds are formed, presenting a different array of
pollutants than have been dealt with in the past.

     We believe the air pollution problems may be particularly
serious.  The synthetic fuel industry is expected to produce
a wide range of air emissions with potentially adverse environ-
mental effects if not adequately controlled.  Oil shale retorting,
for example, will emit nitrogen oxides, sulfur oxides, reduced
sulfur species, ammonia, various volatile and partially oxidized
organics and, of course, particulate matter.  The Prevention of
Significant Deterioration increments available may well pose
serious problems.  The air pollution problems associated with coal
gasification and liquefaction are similar in many ways to those for
oil shale.  These processes can generate significant quantities of
particulates, sulfur compounds, trace metals, high molecular
weight hydrocarbons and nitrogen oxides, etc.  The sulfur species
may be particularly troublesome.

     Water-related environmental problems from synfuel production
may be just as complex.  The oil shale industry will need copious
water supplies for cooling compaction of spent shale, and for
revegetation of surface mined areas.   Coal mining and coal conver-
sion will also have substantial water requirements for process
uses and revegetation.  Supply of water for these activities will
be particularly crucial at some sites in the arid western part of
the country where oil shale retorting and some mine-mouth coal
conversion will occur.  At other sites, mine dewatering and retort-
produced water from shale oil production will produce excess water.
Among the water pollution problems of concern, spent shale, if not
properly handled, could create serious water quality problems from
the leaching of soluble contaminants into nearby ground or surface
water.  With underground, modified "insitu" operations being
considered for oil shale, and possibly for coal, the opportunity for
groundwater contamination is even more likely than for surface
operations.  Here again, the problem is particularly serious in
the western part of the country where groundwater is a vital resource.
From all types of synthetic fuel operations, raw process water
discharges will be highly contaminated by toxic materials (most likely
including carcinogens, mutagens, etc.) which would represent major
threats to both surface and groundwaters if not properly controlled.
It is expected that synfuel facilities will utilize process water
recycling to a great extent but this may not totally solve the water
pollution problems at all locations.

     There are a variety of synfuel-related solid waste problems as
well.  Both oil shale mining and coal mining produce enormous amovats
of solid waste.  Many of the mining problems are similar to those
                             41

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     encountered with conventional coal  mining  and  can be solved
     similarly.   Surface reclamation techniques for strip mined
     areas are particularly successful at  least where an adequate
     water budget exists.   The solid residues of oil shale retorting
     and coal conversion are,  however, another  problem.   Shale oil
     production, for example,  produces spent shale  that is greater
     in volume than the shale  originally removed from the ground;
     coal conversion technologies, both  gasification and direct lique-
     faction, will produce vast quantities of ash.   Each of these
     wastes will most likely contain a wide variety of potentially
     harmful components and will have to be properly managed.   Some
     special wastes from synfuel plants  such as spent catalyst from
     coal conversion may be classified as  "hazardous" under the
     Resource Conservation and Recovery  Act.

          There  is also concern about the  possible  toxicity of liquid
     synthetic fuels themselves, both from the  handling and usage
     standpoints, including concern for  both industrial employees and
     the general public.  Coal-derived liquid fuels,  particularly those
     produced by direct liquefaction, are  of the most concern.  These
     liquid fuels are not of the same composition as  ordinary  crude oil
     products.  They are higher in nitrogen content,  yielding  higher
     NOX levels  upon combustion and they tend to contain more  substances
     which are potentially mutagenic or  carcinogenic  so that public
     exposure to them through  normal usage might represent a significant
     health problem.  More data are needed., however,  on both conventional
     petroleum products and synthetic fuels in  this regard.
oo Pollution Control Guidance Documents  - Part  Of  The Agency's  Regulatory
     Strategy

          Regulating new,  presently non-existent energy  industries,  of
     course, presents different  problems from regulating long-standing
     segments of United  States industry.  The differences are of  such
     an extent that a unique  regulatory  approach is  demanded.   The
     differences arise primarily from  the facts that the new energy
     industries are,  for the  most part,  not  yet commercialized  in the
     United States, have potentially different  effluents and emissions
     from those from existing pollution  sources and  are  being developed
     on a telescoped.time  frame  under  a  governmentally-mandated response
     to "the energy crisis."

          Because of  these circumstances, the general approach  we are
     taking is to issue, as preregulatory multi-media guidance, a series
     of Pollution Control  Guidance Documents, PCGDs—one for each of the
     major energy technologies.   The focal point of  each PCGD is  to  be a
     set of available control alternatives for  each  environmental discharge
     (again, for all  media) along with associated  performance expectations
                                 42

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     and the basis for the alternatives  presented.   The intent  is  to
     present guidance for plants of  typical  size and for each signifi-
     cantly different feedstock likely to  be used.   PCGDs will  not have
     the legally binding authority of regulations but each will be
     reviewed extensively both within and  outside of EPA.  These documents
     will provide useful and realistic guidance to  permit writers  within
     EPA and the States and to the energy  industry  itself during its
     formative stages.  As the energy industry develops, permits for
     individual installations are being  issued based on best  engineering
     judgment and, as the various PCGDs  become available, permits  will be
     prepared in light of the information  the PCGDs contain.  Then, as the
     energy 'industries mature and as .large-scale control technology data
     become available, EPA will invoke its legally-binding regulatory
     procedures, but in a coordinated, multimedia fashion; in the  water
     quality area, for example, this would mean the issuance  of effluent
     guidelines and establishment of appropriate water quality  standards,
     including consideration of related  air  quality and hazardous  waste
     requirements.
oo Processes To Be Covered

          Although the major objective of a PCGD is  to  recommend  pollution
    control options, it will contain a great deal of background information
    on the energy processes themselves and on process streams  and pollutant
    concentrations, and will, on the basis of a series  of  "case studies,"
    offer specific technology-based control guidance for various  kinds  of
    energy processes.  Processes to be included will cover those  that are
    expected to be built for demonstration or commercial application first.
    (Table 2 shows planned process coverage for the  four PCGD's currently
    being written).  It is intended that discussion  of  product (e.g., low
    Btu coal gas) uses also will be included if use  is  integral with the
    manufacturing process.  The process descriptions will  detail  the key-
    features of each process and their pollution potential.  If various
    process modifications are likely to be used, the changes in process
    configuration will be covered and expected changes  in  pollutant
    releases will be indicated.  Pollutant releases  that vary  non-linearly
    with plant size or flow rates will also be identified  and  quantified
    to the extent possible.

          The environmental control alternatives to  be  considered will
    include both end-of-pipe treatment techniques and process  changes.
    Candidate control alternatives will be identified from existing
    United States and foreign bench-, pilot- and commercial-scale
    facilities or from different United States or foreign  processes
    that have similar discharges.  Performance and design  will be
    included as will information on capital, operating  an  annualized
    costs.  Energy usage for control alternatives will  also be included.
    Finally, techniques for monitoring control performance will be
    identified.  The source of all data will be clearly referenced to
    allow referral to original sources;  uncertainties in the data will  be
    indicated.
                                  43

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                     TABLE 2


TECHNOLOGIES FOR WHICH PCGDs ARE CURRENTLY PLANNED



      Indirect Liquefaction

        Lurgi
        Texaco                     Gasifiers
        Koppers Totzek (K-T)

        Fisher Tropsch
        Mobil-M                    Conversion Systems
        Methanol


      Oil Shale

        Occidental
        Rio Blanco
        Lurgi
        Paraho
        Union
        Colony


      Lou Btu Gasifiers
        -single bed, atmospheric, entrained
         gasifiers with and without sulfur control
      Medium/High Btu Gasifiers

        Lurgi
        K-T
        Texaso
        Others to be decided
                        44

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oo Penult Processing

          Various action's have been taken which are aimed at expediting
    permits on energy facilities issued by EPA.  We have set up our own
    Permits Coordination Group to carefully track permits on all energy
    installations, including the important synfuels ones.  The Group
    will identify potential processing problems early and enable
    appropriate remedial action to be taken almost immediately.  We have
    designated a single person in each of our Regional Offices to serve
    as a special point of contact for new energy facilities.  These
    individuals have responsibility for assuring that timely review of
    permits for new energy facilities takes place, that industrial permit
    applicants are well informed as to when EPA will make decisions.
    Industry, especially the small and medium-sized firms, has responded
    very positively to this concept.

          We now set target dates for permit processing based on the
    requirements of individual permit applications.  The complexity of
    individual cases varies considerably and by tailoring the review
    schedule to each individual case, a much shorter average turn-a-round-
    time can be achieved than if a general schedule sufficient for all
    applications is used.  For surface water discharge permits involved
    with surface mining of coal, a memorandum of understanding is being
    developed with the Department of the Interior's Office of Surface
    Mining (OSM) .  With this arrangement, OSM could issue a single permit
    under an agreement with EPA that OSM's comprehensive review procedure
    would also meet EPA's legislative requirements.

          EPA has already issued several air pollution control permits for
    oil shale development.  This early group of permits includes the Colony
    Development Operation of Exxon and TOSCO Corporations, the first
    commercial-scale shale retorting facility for which a permit has beer.
    granted in the United States.  EPA's permit will eventually allow Co_o.Ty
    to expand and produce 46,000 barrels per day of low sulfur distillates
    and other by-products.  The permit will also allow Colony to construct
    and operate:  (1) a 66,000-ton/day underground oil shale mine, (2) a
    surface oil shale retorting facility and (3) extensive support facilities
    including a 194-mile pipeline and a loading terminal.  PSD permits have
    also been issued for the non-commercial-scale projects of Union Oil,
    the C-b tract (Occidental and Tenneco), and Rio Blanco (Gulf and Standard
    of Indiana).  Another synthetic fuels facility which has received
    a PSD permit is the Great Plains Gasification Associates Coal gasification
    plant in North Dakota.  This commercial facility will produce 125
    million standard cubic feet per day of high Btu synthetic fuel gas.

          Finally, a recent development in regulatory procedures to expedite
    permitting is the Consolidated Permit Program (4).  The new consolidated
    permit regulations combine the requirements for the following five
    programs covered under four different Federal environmental laws:
                                   45

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          o   the National Pollutant Discharge  Elimination System (NPDES)
             program of  the  Clean Water Act;
          o   the Prevention  of  Significant Deterioration (PSD)  program of
             the Clean Air Act  (but only where EPA itself is  the permitting
             authority and only to specify permit  procedures);
             Drinking Water  Act (SDWA);
          o   the Hazardous Waste Management program under the Resource
             Conservation and Recovery Act (RCRA);and
          o   the Dredge  and  Fill (Section 404)  program under  the Clean Water Act

    The consolidated permit  regulations and associated application forms
    provide  a framework  for  simultaneously processing multiple EPA permit
    applications for the same facility.  Standard  information can be
    provided on a  single form along with information required for specific
    permiting activities.  Also, where appropriate,  EPA has the ability
    to consolidate draft permits, public notices,  public hearings and
    administrative records for  all permitting  activities for  the facility
    or activity.   These  procedures should not  only expedite the permitting
    process  but also provide an opportunity for better comprehensive
    assessment of  multimedia environmental control.   The results should be
    more consistent and  more efficient control requirements.
THE RESEARCH PROGRAM

          EPA1s energy and environmental  research  program is  based on the
    belief that increased domestic  energy production need not come at the
    cost of a deteriorating environment and  threats to  public health and
    welfare.  The Federal Interagency  Energy/Environment  Research and
    Development Program was established to provide the  information necessary
    to develop a scientific rationale  for policies that strike a balance
    between ample domestic energy production,  reasonable  cost and
    environmental quality.   This interagency effort is  divided into two
    major research programs:   health and  environmental  effects,  and control
    technology.

          The health and environmental effects program  is designed to
    identify energy related pollutants in the  environment,  the mechanisms
    by which they move through the  environment and their  resulting effects
    on human, animal and plant populations.

          The control technology program  provides  information on the types
    and quantities of pollutants released by energy supply activities and
    develops, or stimulates the development  of,  control options where
    necessary.   A major thrust of research in  the  control technology program
    is the generation of technical  and cost  information on which reasonable
    environmental standards can be  based.

          EPA's research program emphasizes  the  generation of data
    necessary to support the establishment arid implementation of technology-
    based environmental guidelines.  This information will be used to assist,
    and ultimately minimize,  environmental damage  resulting from a broad
                                 46

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     of energy fuels  and processes.   Those systems judged  to  have  the
greatest potential for  near-tearm negative impact  will  receive study priority.

          Over the next five years,  the focus of  the research program will  be
on the current and projected coal fuel and oil shale cycles.   Over the  next
fifteen years, coal and oil shale production and use are expected  to grow
faster than any other fuel source, and they both demonstrate  the potential
for creating major environmental problems throughout the fuel cycle.  In
addition, coal is expected to be the dominant fuel employed for electricity
production and will be used increasingly as a feed stock for  synthetic
liquids and gases.
                                       47

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                            FGD  ECONOMICS  IN  1980
                                     By

      G.  G. McGlamery,  W.  E.  O'Brien,  C.  D.  Stephenson,  and  J.  D.  Veitch
               Division of Energy Demonstrations  and  Technology
                                Office of Power
                           Tennessee  Valley  Authority
                             Muscle Shoals,  Alabama
                                  ABSTRACT
      Presented  in this  paper is  a review of  recent  results  from EPA-
 sponsored flue  gas desulfurization and  byproduct/waste  disposal economic
 evaluations prepared by TVA.   Included  are a summary  of comparative capital
 investments and annual  revenue requirements  from a  three-phase  effort  to
 evaluate the leading FGD processes,  and similar  results from three phases
 of sludge disposal studies.   Data from  a 1985 projection of FGD byproduct
 sulfur/sulfuric acid marketing potential are given.

      A new series of FGD process evaluations is  also  previewed  including
 a set of updated evaluation  premises which will  be  utilized in  the early
 1980's.   Examples of the effects of the revised  premises on limestone
 scrubbing economics are shown.   Finally, results are  provided from a recent
 evaluation of limestone scrubbing in a  spray tower  using adipic acid,
 forced oxidation, and gypsum disposal by stacking.
Preceding page biank
                                      49

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                           FGD  ECONOMICS  IN 1980
INTRODUCTION

     Through the publication of numerous  studies  sponsored by EPA and
other organizations,  a great deal of understanding and a broadened
perspective of FGD economics have been developed  during the past decade.
As we enter the 1980's, interest in FGD economics continues as strong as
it was 10 years ago.   Changes in technology,  environmental regulations,
economic conditions,  and design philosophies  all  affect the projection
of FGD economics to such an extent that constant  reassessment is necessary.
Neither the pace nor the effects of these changes can be expected to
diminish soon.

     The interagency EPA-TVA program to evaluate  FGD economics that began
in 1967 is now well into its second decade of activity.  Projects to
evaluate the economics of leading nonrecovery and recovery FGD processes,
waste disposal processes, coal-cleaning systems,  and byproduct marketing
studies have all been a part of this program.  Results from much of this
work have been reported at earlier symposiums.

     During 1980, additional results have been derived from the continuing
program.  This paper summarizes most of the recent published data and
work in progress.  First, a summary of results from three reports on
comparative FGD process economics is presented.   Second, a summary of
information from three published reports  on sludge disposal economics is
given.  All six of these reports utilize  the  same time frame (1977-1980)
and design and economic premises.  Reported next  are the data from a
1985 projection of FGD byproduct sulfur/sulfuric  acid marketing.

     A new series of FGD process evaluations  was  begun in 1980 using an
updated set of design, regulatory, and economic premises more typical of
conditions to be faced in the early 1980's.  Evaluation projects using a
costing time frame of 1981-1984 are previewed on  dry scrubbing processes,
limestone process alternatives, gypsum-producing  processes and ash
disposal systems.  The new premises are also  described, as is a stepwise
conversion of limestone scrubbing economics from  the old premises to the
new premises.

     In the final portion of the paper, results are projected for an
advanced limestone scrubbing process using a  spray tower, adipic acid
additive, forced oxidation, and gypsum stacking.   This particular evalua-
tion is for a limestone system expected to come into common usage in the
future if scheduled large-scale process development is successful and
environmental acceptability is proven.
                                     50

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     Because the results presented herein are from a variety of studies
using different premises, special  caution should be exercised in utilizing
the results.  Particular attention should be paid to the different
designs evaluated for the limestone scrubbing process.
FGD ECONOMIC STUDIES

     In 1977 TVA began a series of FGD economic studies designed for the
twofold purpose of updating previously evaluated processes and integrating
evolving technologies into the EPA-TVA FGD economic studies.  Three
reports (1,2,3), two of which have been published, covering seven FGD
systems and two processes for producing sulfur from FGD S02, have been
prepared.   The limestone and lime scrubbing processes were updated from
an earlier report, as were the magnesia and Wellman-Lord scrubbing
processes (4).  A generic double-alkali process was included to represent
this important type of nonrecovery FGD process.  The citrate process and
the Rockwell International aqueous carbonate process (ACP) were included
as emerging sulfur-producing processes.  The ACP represents two areas of
new FGD technology, spray dryer FGD and the use of coal as a reducing
agent to produce sulfur.  The latter technology was also represented in
this series of studies by the Foster-Wheeler Energy Corporation Resox®
process and the Allied Chemical coal/S02 reduction process, both of
which utilize coal to produce sulfur from S02-  Schematic flow diagrams
of all the processes evaluated in this series are shown in Figure 1.

     These processes represent a range of development from established
technology (the limestone and lime), through demonstration and recent
commercialization (the double-alkali, citrate, magnesia, and Wellman-
Lord scrubbing processes), to less-developed processes (the ACP and the
Resox® and Allied coal reduction processes).

     The same premises, based on a 500-MW power plant burning 3.5%
sulfur coal, meeting the 1.2 Ib S02/MBtu NSPS, and using mid-1979 capital
costs and mid-1980 annual revenue requirements, were used throughout.
As in other EPA-TVA economic studies, these base-case conditions were
systematically varied to evaluate different fuel, power plant, and FGD
conditions.  In all, over 100 case variations of 9 basic FGD processes
were evaluated.  In addition, in recognition of the growing importance
of energy in design considerations, a ground-to-ground energy evaluation
was made for some of the processes.

Prbcess Descriptions

     The limestone, lime, and double-alkali processes produce a waste
slurry that is disposed of in a pond.  In the limestone process the flue
gas is scrubbed with a slurry of ground limestone, forming calcium
sulfur salts that are discarded by pumping a purge stream to a disposal
pond.  The lime process is similar except that a slurry of lime, is used
as the scrubbing medium. .In the double-alkali process a solution of
                                     51

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        LIMESTONE  S LIME  PROCESSES

                          SCRUBBER
 FLUE.
  GAS
ESP




,,
1
, 	 , f"\ ? 	 *• TO STA
RFHFAT ~J

	 	 	 i iMr^Tnwr
0, iiDRY ^— LIMLo ' UNL
* PREP. UK L'ML
i >
1 	 L-t) s-^l
                                                           POND
       DOUBLE-ALKALI  PROCESS
                         SCRUBBER
 FLUE
 GAS

ESP





w























\
REHEAT
f~'
^ ABSORB.
"• REGEN ""

A I
T 1
1 <\T-
-^— ~
Ja2C03
, SLURRY
PREP




•• IU 3 IA

m LIME
OR



1
                                                           POND
       MAGNESIA  PROCESS
                       PRE-
FLUE _^« 	
GAS ^t 	
ESP
w yv >
s


CRUBBER SCRUBBER







4 	
REHEAT


SLURRY
PREP.
                                                        •TO STACK
                                                  MgO MAKEUP

                     CHLORIDES
1
DRYER


i
*MgO
CALCINER
so2


ACID "1
PLANT j
       WELLMAN-LORD  PROCESS
FLUE
GAS
            ESP
                       PRE-
                     SCRUBBER  SCRUBBER
                                    _NQ2S03
                     CHLORIDES
                                [SULFATE
                                I  PURGE
 EVAR
REGEN.
             •TO STACK
         •Na2CO,
  TO END PLVJ
(ACID FLAMT, RL'
 OR AL- 'iLLi C\
Figure 1.  FGD process flow diagrams.
                               52

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               CITRATE   PROCESS

                             SCRUBBER
                                                      TO STACK
                                                           Na2S04
      GAS
                              CHLORIDES
               AQUEOUS  CARBONATE  PROCESS
                                       Na2C03  SOLUTION
CYCLONE SPRAY DRYER 1
rLUt * 	 	
GAS ESP
V L J
Y ^^^ .
FLY ASH
W!
RESOX UNIT
R
ANTHRACITE — *
S02 — *
_£_\ 	 y-^-TO STACK
CO/
T
rRE;

P
C/l
•— *01
\L r^pf
1


1 L
RE- — '

•F GAS ..CHLORIDES
ACCESS, a SOLIDS
*C02
fc CARBON.
DECOMP.

H2S
CLAUS


/

Na2C03
— *• SULFUR
*
SOLIDS
E ACTOR
•
»
— *• CONDE
	 fcTAIL GAS
.N. TQ FGD
SULFUR
                                    Y
                                    CHAR
               ALLIED  UNIT
            COAL-
                                L»J   I  m
                         REACTOR r\  )
Figure 1  (continued)
                            f
                           S02
                                 SOLIDS
CLAUSTL^TAIL GAS
 UNIT  |  TO FGD
                                                           SULFUR
                                53

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sodium sulfite is the scrubbing medium.   The spent solution is regenerated
by adding lime, producing calcium sulfur salts that are discarded^in a
disposal pond.  A slurry of magnesium oxide is used as the scrubbing
medium in the magnesia process.  The spent slurry is dewjatered, dried,
and thermally decomposed to regenerate the magnesium oxide and produce
SO-> which is converted to sulfuric acid in a conventional acid plant.
  Z,                                                     i

     The citrate process is a wet scrubbing process usinfe a sodium
citrate solution as the absorbent.  The absorbent is regenerated and the
SOX compounds reduced to elemental sulfur by liquid-phase reduction
using H2S.  The H2S is produced by reducing some of the product sulfur
using natural gas.

     In the Wellman-Lord process a solution of Na2S03 is the scrubbing
medium.  Reaction with SOX produces NaHSC>3 which is heated to evolve SC>2
and regenerate Na2SC>3.  Other sodium compounds, primarily Na2S04, form
and must be removed.  Unlike the magnesia process, which produces a
dilute S02 off-gas, the Wellman-Lord process produces an SC^-rich off-
gas more suitable for direct reduction to sulfur.  In these studies it
is evaluated with a sulfuric acid end plant and with the Resox" and
Allied coal reduction processes.

     The Resox® process consists of a vertical reactor through which
rice-sized anthracite flows by gravity at a controlled rate.  The S02~
rich off-gas is mixed with controlled amounts of water and air, heated,
and passed through the reactor.  In a complex series of reactions some
anthracite is oxidized to maintain the reaction temperature and most of
the SC>2 is reduced to sulfur.  A noncaking coal such as anthracite is
necessary.  Careful control of residence time, temperature, and SC^rl^O
ratio is necessary to limit the thermodynamic tendency of the sulfur to
go to H2S.  Sulfur is condensed from the emerging gas and the remainder
is burned to convert the sulfur compounds to SC>2 and returned to the FGD
system.

     The Allied process uses a slightly pressurized fluidized-bed reactor
containing a mixture of ground power plant coal and silica sand through
which the SC>2 off-gas, mixed with a small quantity of air, is passed.
Most of the SC>2 is reduced to sulfur but appreciable H2S is also produced.
The off-gas is passed through a particulate collector, a liquid sulfur
scrubber to condense the sulfur, and a Glaus unit to oxidize the'l^S to
sulfur before the residue is incinerated and returned to the FGD system.
The process also includes coal drying and grinding facilities and sulfur
cooling and filtration facilities..

     The ACP consists of spray dryer absorbers using a soda ash solution
followed by ESP's to collect the sulfur salt particulate matter and
residual fly ash not removed in upstream cyclones.  The particulate
matter is mixed with ground power plant coal and injected into refractory-
lined reactors.  Air is injected to maintain a reaction temperature of
1500°F, at which the sodium salts are molten.  Most of the sulfur is
reduced to the sulfide.  The reactor off-gas is scrubbed to remove
                                     54

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chlorides and ash and used as a CC>2 source.  The melt overflows to a
quench/dissolving tank.  The dissolved melt is treated with process
to form NaHS and then with process C02 to produce H^S and NaHC03, which
is further reacted with C02 off-gas to produce Na2C03-  The H2S is
processed to sulfur in a conventional Glaus unit.

Economic Results

     The base-case costs for each of the nine processes are shown in
Table 1.  Except for the AGP, the costs are product-related, falling
into separate groupings of waste-, acid-, and sulfur-producing processes
in both capital investment and first-year revenue requirements.  The
differences in cost between the waste-producing and acid-producing
processes are essentially the costs for absorbent regeneration; ponding
costs and acid plant costs do not differ greatly and raw material costs
do not differ sufficiently to produce large cost differences.  The
higher costs for sulfur-producing processes are the result of the added
costs for reduction of sulfur oxides.  Here coal reduction holds a
strong advantage over other fossil reducing agents.  In the citrate
process, 16% of the annual revenue requirements  (1.06 mills/kWh of 6.44
mills/kWh) are for natural gas to produce H2S.  In contrast, reducing
coal costs range from 9%  (Resox®) to 4%  (Allied).
                  TABLE 1.  FGD PROCESS ECONOMIC COMPARISONS
                                                   Mid-1980 first-year
                                Mid-1979 capital   revenue requirement,
                                investment, $/kW	mills/kWh	
     Waste-Producing Processes

     Limestone                          98                 4.02
     Lime                               90                 4.25
     Double alkali                      101                 4.19
      Sulfuric Acid Processes

      Magnesia   .                        132                 5.08
      Wellman-Lord/sulfuric acid         131                 5.11
      Sulfur Processes

      ACP                                119                  4.81
      Wellman-Lord/Resox                 138                  6.03
      Wellman-Lord/Allied                141                  5.94
      Citrate                            143                  6.44
                                     55

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     The anomalous capital investment of the ACP results from a credit
for the unnecessary separate fly ash ESP's and from the intrinsic chloride
purge from the reducer off-gas quench.  If no ESP credit is given (as in
an existing plant with ESP's in place) its capital investment becomes
137 $/kW.  Similarly, if no chloride removal is necessary in the wet
processes, these process costs are reduced about 10 $/kW.  Under these
conditions, the ACP becomes the highest in capital investment.  Specific
power plant conditions are thus important in the comparative capital
investments of the regeneration processes.  In first-year revenue require-
ments the lower costs for the ACP are less site specific.  It has low
raw material costs and low utility costs that prevail regardless of
specific fuel and power plant conditions.

Ground-to-Ground Energy Assessment

     As a part of this series of FGD studies, a ground-to-ground energy
assessment of the limestone, lime, and magnesia processes was made.
This consisted not only of the FGD energy requirements but the energy
consumed in mining, processing, and transportation of the raw materials,
the disposal of wastes, and an energy credit for the sulfuric acid
produced.  The assessment represents, in a sense, the energy removed
from a hypothetical energy reservoir because of the operation of the FGD
systems.  A credit is given for the sulfuric acid because it replaces
acid that would be produced from sulfur, and thus the energy that would
have been  consumed in mining and transporting the sulfur and producing
the acid.  The results are shown in Table 2 and Figure 2.
          TABLE 2.  FGD GROUND-TO-GROUND ENERGY REQUIREMENTS
                                     Btu/lb sulfur removed
Function
Mining
Absorbent processing
Transportation
FGD
Waste disposal
Total
Byproduct credit
Net total
Btu/kWh
% gross power unit output
Limestone
438
176
14,042
22
14,678
_
14,678
291
3.2
Lime
356
6,198
143
13,165
15
19,877
_
19,877
395
4.4
Magnesia
25
161
33
26,387
26,658
(5,491)
21,115
420
4.7
                                     56

-------
   30-
  20-
$
o
i
r
<0
i
0-
   10-
              ABSORBENT
                  I  I
                                     BYPRODUCT
                                      CREDIT
         Limestone    Lime     Magnesia
 Figure 2.  Ground-to-ground energy requirements for
          limestone, lime, and magnesia scrubbing
          processes.
                       57

-------
     The ground-to-ground energy comparison shows considerably different
relationships than comparison of FGD energy requirements alone.  The FGD
energy requirements of the magnesia process (typical of regeneration
processes) are about twice those of the limestone and lime processes.
The.absorbent energy requirements are low for the magnesia process
because only makeup magnesia is used.  In contrast, the lime process,
which has the lowest FGD energy requirements, has much higher energy
requirements when the energy for calcining lime is included.  With the
byproduct credit included, the magnesia process is not appreciably more
energy intensive than the lime process.

     Energy requirements cannot, of course, be directly related to FGD
costs.  Energy consumed in absorbent production and transportation, for
example, is seen only indirectly, as it affects raw material costs.  In
addition, the form of the energy may have an important effect on costs.
The magnesia process uses fuel oil for over one-third of its energy
requirements whereas almost all of the limestone and lime energy
requirements are met with coal.  The significance of these differences
on  costs is dicussed further in the byproduct marketing portion of this
paper.
FGD WASTE DISPOSAL ECONOMICS

     Also during the past three years, TVA has conducted a series of
evaluations for EPA on the economics of disposal processes for flue gas
cleaning wastes.  The first three studies (5,6,7) deal with the disposal
of fly ash and scrubber wastes from limestone/lime FGD systems.  In all,
seven disposal methods were evaluated covering a range of existing or
potential disposal options of the late 1970's.  All of the evaluations
were based on the same premises, using as the basis a 500-MW power plant
burning a 3.5% sulfur eastern coal and scrubbing with a limestone slurry
to meet the then-existing 1.2 Ib S/MBtu NSPS.  In addition, over 175
case variations representing various power plant, fuel, waste treatment,
transportation, and disposal site conditions were evaluated.  Schematic
flow diagrams of the processes are shown in Figure 3.

     Except for the gypsum process, the scrubber waste consists of a 15%
solids slurry with a sulfur species composition of 85% CaS03'l/2H20 and
15% CaSQ4'2H20.  Fly ash is included in the slurry except for the
sludge - fly ash blending and Dravo landfill processes.  In dewatering,
30% solids from the thickener and 60% solids from the filter is used.
For the gypsum process essentially all the sulfur is CaS04'2H20 and the
filtered solids is 80%.

Process Descriptions

     The untreated ponding case assumes that the effluent is pumped
directly to an earthen-diked pond.  The Dravo, IUCS, and Chemfix processes
are all commercial fixation processes using somewhat different approaches
to treat dewatered FGD sludge.  All depend on additives that produce
                                     58

-------
UNTREATED  PONDING
DRAVO PONDING


THICKENER

CALCILOX
»-



1
LIME

MIXER

IUCS

THICKENER


FILTER


MIXER
                                                              LANDFILL
CHEMFIX


THICKENER



CEMENT

FILTER




1
r
SILICATE

MIXER I +


SLUDGE- FLYASH BLENDING ^

THICKENER


FILTER
&.

MIXER
                                                               LANDFILL
GYPSUM

AIR
OXIDATION


THICKENER


FILTER

	 "
                                                               LANDFILL
MINE DISPOSAL
                                                            ~~j  MINE  j~
DRAVO LANDFILL
                                                               LANDFILL
Figure 3.   Process flow diagrams.
                                   59

-------
cementitious chemical reactions.  The types and quantities of the
additives and the degree of dewatering can be controlled to produce a
soillike material over a curing period of hours or months.  The Dravo
process uses their product Calcilox,® a processed blast furnace slag,
sometimes with lime or fly ash, or both.  Depending on the degree of
sludge dewatering and materials added, the treated material is pumped to
permanent or temporary pond storage or it is hauled to disposal after a
curing period.  The IUCS process uses lime and fly ash blended with
dewatered sludge to produce a soillike solid.  The Chemfix process uses
Portland cement and sodium silicate blended with dewatered sludge to
produce a soillike solid.  The process is said to provide an encapsula-
tion that reduces leaching.  For comparison, a sludge - fly ash blending
process without purchased additives, is included.  The gypsum process
differs in that air oxidation equipment is added to the scrubber loop,
permitting production of the more easily dewatered and denser CaS04«2H20.
It is assumed this material can be dewatered and handled as a solid
without stabilization or fixation with additives.  Finally, a process
using the sludge - fly ash blending process with disposal in a surface
mine is evaluated.

Economic Results

     Cost breakdowns of the base cases by processing areas were made, as
shown in Table 3, to facilitate identification of cost elements and
comparison of different disposal processes.  The sludge - fly ash blend-
ing process, the mine disposal process, and the Dravo landfill process
require inclusion of ESP costs for comparison with the other processes.

     In those cases in which fly ash is collected separately the cost of
ESP units and their operation is a major component of the waste disposal
costs.  In comparison, simultaneous fly ash removal results in relatively
modest increases in thickening and filtration costs.  Separate collection
of fly ash is, of course, possible with all of the processes evaluated
and would require similar costs for all processes.  In comparison of
landfill disposal practices having separate fly ash collection, cost
differences would largely be reduced to the raw material portion of the
cost breakdown.

     For the processes using purchased fixatives, raw materials are an
important element of both capital investment and first-year revenue
requirements.  Fly ash handling is also a relatively expensive element.
The advantage of a single fixative is illustrated by comparison of raw
material costs for processes that use two additives with processes that
use one.   Thickening is the largest capital investment cost element,
excluding ESP costs, for all of the nonponding processes.  It is also a
large cost element in annual revenue requirements.  Filtration is also
a large cost element, though considerably less so than thickening.
Dewatering costs for the gypsum process are lower than the other simul-
taneous fly ash - FGD waste filtration processes because of the predicted
superior filtration characteristics of the high-sulfate sludge.  Mixing
costs are a minor part of both capital investment and annual revenue
requirements.
                                    60

-------
TABLE 3.  MODULAR COSTS BY PROCESSING AREA FOR EIGHT DISPOSAL PROCESSES
Capital investment by processing
Other Raw materials
Ponding
Dravo ponding
IUCS
Chemf ix
Sludge-fly ash
Gypsum
Mine disposal
Dravo landfill


blending 19.
4.
19.
19.


2a
6b
2a
2a
9.0
4.2
8.5
4.4

4.4 .
6.2
Thickening Filtration
8.4
8.5
9.1
6.3
5.2
6.2
6.0
First-year revenue


Ponding
Dravo ponding
IUCS
Chetnfix
Sludge-fly aeh
Gypsum
Mine disposal
Dravo landfill






blending 0.
0.
0.
0.






56S
29d
56C
56C



0.91
0.44
0.97
0.22

0.22
0.57



0.24
0.29
0.29
0.24
0.29
0.25
0.22
4
4
2
3
2
2
.1
.8
.5
.0
.5
.2
requirements




0
0
0
0
0
0




.18
.19
.11
.16
.11
.10
area, $/kW

Mixing Storage Disposal
1
0
1
1
0

0
0
.4
.5
.1
.6
.9

.9
.8 1.1
by processing area


0
0
0
0
0

0
0


.14
.03
.06
.06
.05

.05
.05 0.03
33.0
30.3
3.5
3.1
3.1
2.6
2.0
3.8

Total
34.4
48.2
21.4
27.1
36.4
15.4
35.3
39.4








, mills/kWh


0.80
0.74
0.54
0.49
0.45
0.44
0.36
0.47


0.94
1.91
1.51
2.00
1.64
1.18
1.54
2.00
$/ton
dry waste
8.1
15.3
12.6
15.9
9.3
7.9
8.2
11.9

Basis: 500-MW
power plant,
removal in scrubber
127,
500-hour life
where cost is not
, 7,000 hr/yr revenue requirement basis; 3.
shown. Limestone
scrubber,
5% S, 16%
1.5 stoichiotnetry, 15%
ash coal; fly ash
solids
waste to
disposal system.
a. $9,614,000
b. $2,3u3,000
c. $1,975,000
d. $1,005,000
ESP cost for
separate fly ash
collection.







air-oxidation modifications.
ESP operatJi.^
costs.
air-oxidation ope.
rating c^sts









-------
     Transportation and disposal site costs illustrate fundamental
differences between ponding and landfill disposal methods.  Capital
investment for ponding transportation and disposal site costs is an
order of magnitude greater than the capital investment for landfill
transportation and disposal site operations.  Capital investment for
transport lines is also an important element in ponding.  Among the
landfill and mine disposal processes, transportation and disposal site
costs are a relatively minor element of total capital investment.

     First-year revenue requirements for ponding transportation and
disposal site costs are also higher than those for landfill and mine
disposal although the differences are less pronounced.  About two-thirds
of the annual revenue requirement direct costs for ponding transportation
and disposal site operations consist of pond maintenance.  Transportation
of the waste is a relatively minor cost element.  In contrast, about
four-fifths of the annual revenue requirements direct cost for landfill
and mine disposal transportation and disposal site operations is for
labor and supervision, much of it for loading and hauling.

     In overall comparison of the processes evaluated, the most important
capital investment cost elements are separate fly ash collection, raw
material handling, thickening, and pond construction.  Large cost elements
in first-year revenue requirements are separate fly ash collection, raw
material purchase and handling, and disposal.

     The most important variations from the base-case conditions affecting
costs are power plant size, coal sulfur and ash content, and transportation
distance to the disposal site, as shown in Figure 4.   Coal sulfur content
affects costs both through the volume of waste to be processed and
disposed of and, for processes using fixatives, the quantity of fixative
required.  Costs for the disposal processes increase at different rates
with increasing sulfur content, depending on the relative influence of
these factors.  Fixation processes increase in cost more rapidly than
the processes that do not use purchased fixatives.  Distance to the
disposal site illustrates an important difference between the ponding
and landfill processes.  Ponding investment costs increase dramatically
as the distance increases to 5 and 10 miles,  in contrast, transportation
costs for landfill processes decrease more slowly with distance.  The
relatively small cost advantages of mine disposal are lost in higher
transportation costs if the comparison is made between a landfill onsite
and a mine over a few miles from the power plant.  From a purely econom:.c-
viewpoint, mine disposal requires very close proximity of power plant
and mine for its economic advantages to be realized.


BYPRODUCT MARKETING

     The EPA-sponsored FGD byproduct'marketing system began as a limited
production-marketing model for sulfuric acid in the early 1970's (8).
Several expansions of the methodology led in 1978 to the basis of the
present system (9),  a comprehensive analysis of the potential of FGD

-------
                         EFFECT OF POWER PLANT SIZE ON WASTE DISPOSAL COSTS.
                                             EFFECT OF COAL SULFUR CONTENT ON WASTE DISPOSAL
                                             COSTS.
         0.
         ra
         o
            60
            40
            20
                                                                                          60
                                                                                       I
                                                                                          20
                            400
                                            800
                                                            1200
                                                                           1600
OJ
        !f    3
        I
                                              1—Untreated ponding
                                              2—IUCS
                                              3—Sludge-flyash' blending
                                              4—Gypsum
                                              5—DI-HVO landflU
                           400             800

                                   Pn.-p.r plant si:'^, K.i
^\	
 1200
	I
 1600
                                                                                       3
                                                                                       o-
                                                                                       s
                                                                                       41
                                                                                       0)
                             CO
                            I
                                             1—Untreated ponding
                                             2--IUCS
                                             3—Sludge-flyash blending
                                             4—Gypsum
                                             5—Dravo landfill
                                          J_
   2           3
Sulfur in coal,  /;
                                                    Ji'!l>., s on disfosal co3t;

-------
             EFFECT OF COAL ASH  CONTENT ON WASTE DISPOSAL COSTS.
60
40
20
                                                            _J
                                                            20
             12
                                  16
                   1—Untreated  ponding
                   2—IUCS
                   3—SJudge-flyash  blending
                   4—Gypsum
                   5—Dravo landfill
             12
                                  I
                                 16
                         Ash  in  coal,
                                                            20
           (co;U
                                                                                           EFFECT OF DISTANCE TO DISPOSAL SITE ON WASTE
                                                                                           DISPOSAL COSTS.
                                                                              80
                                                                              60
                                                                              40
                                                                              20
                                                                                     63==
                                                                                     4
                                                                                                                                           10
1—Untreated ponding
2—IUCS
3—Sludge-fly ash blending
4—Gypsum
5—Dravo landfill
6—Mine disposal
 2            4           6           8

    Distance to disposal site, miles
10

-------
byproduct sulfur and sulfuric acid production and marketing by U.S.
electric utilities.  Basically the system compares low-sulfur fuel and
regeneration and waste-producing FGD costs for existing and planned U.S.
utility power plants, determines FGD byproduct revenue from sales to
U»S. sulfuric acid plants, and determines the mix of strategies that
results in the least-cost option and the highest total revenue from FGD
byproduct sales.  FERC and published utility data, transportation data,
and U.S. sulfuric acid plant data are used.  TVA process economics,
scaled to projected power plant operating conditions, determine FGD
costs.

     An updated projection of FGD sulfuric acid marketing potential for
1983 was published in 1979 (10), as was a users manual for the com-
puterized system (11).  The 1983 projection also contained a manually
prepared forecast of FGD sulfur marketing potential.  Several trends
became apparent in the 1983 projection:  rapidly evolving FGD technology;
disproportionate fuel cost changes, particularly for petroleum products;
changes in historical patterns of utility coal use and sulfur and sul-
furic acid production; and evolving environmental legislation promised
to influence earlier patterns of FGD byproduct production.

    •Developments in FGD, such as the recognition that chloride control
was necessary in some cases for regeneration processes to prevent loss
of absorbent effectiveness, special purge systems, and severe corrosion
problems, altered FGD costs.  New technologies, such as spray dryer FGD
and coal reduction, promised further changes.  The type of fuel used in
the FGD process was also becoming an important economic factor.  The
growing importance of secondary sulfur and sulfuric acid production was
seen to be a potentially important consideration.  Legislation such as
RCRA and the 1979 NSPS revisions, restricting waste disposal options and
the use of low-sulfur fuel, would be important in FGD economics in the
1980*s.  It was also apparent that the usefulness of these projects
would be increased by extending them further into the future, on a scale
similar to the time period required for power plant planning and
construction.

     Beginning in late 1979, a projection for 1985 was started.  Although
a  1990 projection would have been more desirable, availability of data,
particularly on power plant construction, coal use, and fuel costs,
precluded a projection beyond 1985 at that time.  Numerous system changes
were made, including updated FGD technologies (limestone throwaway,
magnesia to acid, and ACP for sulfur), a general updating of power plant,
transportation, and acid plant data, inclusion of a spray dryer FGD
sulfur-producing process, and inclusion of Canadian sour gas sulfur as a
market factor in the upper United States.  The results, which were
published this year  (12), showed a number of changes from previous
projections.

     The combined sulfur and sulfuric acid market for 1985 was projected
to be 165,000 tons of sulfur from 11 power plants and 554,000 tons of
sulfuric acid from 6 power plants.  The total benefits for the electric
                                     65

-------
utility and sulfuric acid industry were about $20,000,000.  The results,
shown in Table 4, differ considerably from the 1983 projection, which
showed 1,200,000 tons of sulfuric acid but no sulfur.

     Several factors are important in both the total FGD byproduct
production projected and the sulfur-sulfuric acid mix.  Most of the
production of both comes from new plants projected for a 1985 startup,
which were assigned to regulation under the 1979 revised NSPS for
modeling purposes.  In addition, inclusion of fixation and landfill
disposal in the limestone scrubbing process, used for the waste-producing
FGD option enhances the FGD byproduct option, although limestone scrubbing
remains the predominate FGD option.

     Sulfuric acid production was reduced by several factors, among
which increased costs for the magnesia process used in the FGD model
were most important.  Inclusion of provisions for chloride control and
the cost of fuel oil in the process were particularly important.  The
increase in potential FGD sulfur production stems largely from the use
of a spray dryer recovery FGD process based on the Rockwell International
aqueous carbonate process.  Reduced costs in the form of simultaneous
fly ash and particulate sulfur salts collection and the use of coal as
the reducing agent, were important factors.  In maximizing the combined
sulfur-sulfuric acid market, all of which is assumed to be sold to
sulfuric acid plants, alternate markets for Sulfur were also more prevalent
than those for sulfuric acid.

     The 1985 projection indicates several factors that will have important
influences on FGD byproduct production by the late 1980's.  Environmental
legislation affecting waste disposal practices and the restricting use
of low-sulfur coal as a compliance strategy could enhance the economic
attractiveness of regeneration FGD processes.  The economics of byproduct
FGD processes that use coal as the fuel in the regeneration-manufacturing
process will be more favorable than those using oil br natural gas.
Similarly, processes that combine flue gas cleaning functions, such 'as
fly ash and sulfur salt collection, will have important economic advantages.

Fuel Oil Price Escalation

     An interesting aspect of FGD economics in the past few years, as
the cost basis has been projected into the 1980"s, is the disproportionate
effect of energy costs.  This is particularly apparent in the byproduct
marketing studies, which are projected further into the future than most
FGD economic studies.  In the 1985 projection a 15% annual inflation
rate for No.  6 fuel oil was used, based on petroleum cost projections
available in early 1980.  As an illustration of the effect of this rate
on costs, equivalent cost increases for fuel oil, natural gas, and coal
are shown below.
                                     66

-------
TABLE 4.  1985 PROJECTION OF THE PRODUCTION AND DISTRIBUTION

               OF FGD SULFUR AND SULFURIC ACID

Power plant location
Sulfur
Staten Island County, NY
Martin County, FL
Washington County, FL
Sherburne County, MN
Westmoreland County, PA
Montgomery County, MD
Shelby County, AL
Williamson County, IL
Rusk County, TX
Henderson County, TX
Armstrong County, PA
Sulfuric Acid
Person County, NC
Jasper County, IL
Pike County, IN
Northhampton County, PA
Delaware County, PA
Titus County, TX
Tons
7,000
28,000
20,000
8,000
24,000
10,000
12,000
11,000
9,000
7,000
29,000
165,000a
103,000
122,000
51,000
182,000
53,000
43,000
554,000b
Consumer location
Newark, NJ
Pierce, FL
Do than, AL
White Springs, FL
Dubuque , IA
North Bend, OH
Copley, OH
Baltimore, MD
Tuscaloosa, AL
East St. Louis, IL
Fort Worth, TX
Fort Worth, TX
Cleveland, OH
Richmond, VA
Wilmington, NC
Norfolk, VA
Tuscola, IL
Indianapolis, IN
Daepwater, NJ
Edison, NJ
Gibbstown, NJ
Gibbstown, NJ
Shreveport, LA
Tons
7,000
28,000
7,000
13,000
8,000
8,000
16,000
10,000
12,000
11,000
9,000
7,000
29,000
165,000a
36,000
26,000
41,000
122,000
51,000
95,000
74,000
13,000
53,OGC
43,000
554,000b

 The potential revenue/savings  to both  industries combined  is
 projected to be as much as $10,000,000 for an approximate
 average of $60/short ton of sulfur.
 The potential revenue/savings  to both  industries combined  is
 projected to be as much as $10,500,000 for an approximate
 average of $19/short ton of sulfuric acid.
                            67

-------
       Annual price
       escalation,  %
                Equivalent  price increase,  1979-1985
               No.  6  fuel oil,    Natural gas,    Coal,
                    $/gal	$/kft3       $/ton
5
15
25
0.20
0.79
1.69
1.37
5.29
11.33
30.13
116.32
249.36
     To equal the price increase projected for fuel oil, for example,
the price of coal would have to increase over 100 $/ton.  Processes such
as the magnesia process that use fuel oil are thus placed at a dis-
advantage compared with processes such as the AGP using coal.

     The effect of fuel oil price escalation on the cost of FGD sulfuric
acid is shown in Figure 5.   The effect is twofold, first in FGD costs
and second in the avoidable production costs to acid producers.  This is
a cost calculated by the byproduct marketing system to determine the
price of FGD acid at each acid plant.   It represents the break-even
point between buying FGD acid to meet  marketing requirements and producing
acid.  In shutting down an acid plant, however, steam production is lost
and normally must be replaced by a boiler.   Because of size, this
logically would be an oil-fired boiler.   High fuel oil price escalation
rates thus decrease avoidable production costs, resulting in the need of
a higher acid price margin to make the purchase of FGD acid economical.
           90
           80
         o:
         <
         5 70
        o
        < 60
        o
        cc
        p 50
        to
H
O
Q
UJ
£E
           3°
           20
           10 -
                 I Increased  FGD Cost

                  Decreased Acid Plant Avoidable Cost
               %
I
                       10.            15,             20
                      FUEL  OIL PRICE  ESCALATION (%) TO 1985
        Figure 5.  Reduction in potential  FGD  sulfuric  acid  margin with
                   No. 6 fuel oil annual price escalation.
                                    68

-------
FGD AND SOLID WASTE PROCESS EVALUATIONS IN PROGRESS

     With the completion of the 1977-1980 series of SOX control and FGD
solid waste process designs and evaluations, plans were made for extension
of the series to other important FGD and waste disposal processes not
yet evaluated.  During the planning cycle, dry scrubbing processes were
just beginning to capture strong interest.  Therefore, the first new
study for the 1980's was a preliminary economic evaluation of this
technology.  The first report on a lime spray dryer system for a western
low-sulfur coal application was published during early 1980 (13).  A
second more detailed report summarizing current dry FGD process technology
and the economics for both low- and high-sulfur coal will be published
soon (14).  T. A. Burnett will present results from these reports in a
paper to be presented later in the symposium.

     A second project is now underway to prepare a report summarizing
the designs and economics of wet limestone-lime processes which have
been studied at the EPA-TVA Shawnee Test Facility.  Thirteen different
process variations included in this report are listed below.

    1.  Turbulent Contact Absorber® (TCA) - Onsite ponding

    2.  TCA - Forced oxidation - Landfill

    3.  TCA - Forced oxidation   Adipic acid - Landfill

    4.  TCA - Forced oxidation - MgO - Landfill

    5.  Spray Tower (ST) - Onsite ponding

    6.  ST - Forced oxidation - Landfill

    7.  ST - Forced oxidation - Adipic acid - Landfill

    8.  ST - Forced oxidation - MgO - Landfill

    9.  Venturi-Spray Tower (V-ST) - Onsite ponding

   10.  V-ST - Forced oxidation - Landfill

   11.  V-ST - Forced oxidation - Adipic acid - Landfill

   12.  V-ST - Forced oxidation - MgO - Landfill

   13.  Venturi - Forced oxidation - Adipic acid - Landfill


The final report should be available during 1981.
                                     69

-------
     A third project,  which is about half completed,  is a study of three
leading gypsum-producing FGD systems.   The Dowa process, which was
developed in Japan on  oil-fired boilers,  is being marketed in the United
States by UOP and has  been tested on a 10-MW prototype at Shawnee, is
one of the processes.   The Saarberg-Holter process,  a German-developed
system marketed by Davy-McKee in the United States,  is the second process,
The third system is a  limestone spray tower using adipic acid addition,
forced oxidation, and  gypsum stacking for waste disposal.  The report
for this project is expected to be ready  for distribution in mid-1981.
There are other gypsum-producing processes being developed for commer-
cial use; it is hoped  that these can be evaluated in a future study.

     The last defined  project now underway in the expanded series is  an
evaluation of ash disposal systems and practices for coal-fired power
plants.  The draft report for this project has been  prepared and publica-
tion is expected shortly.

     The ash disposal  methods evaluated in this study are represented by
five base-case processes based on major utility ash  disposal practices.
Four base cases represent disposal of noncementitious eastern coal ash.
They consist of (1) direct sluicing of combined fly  ash and bottom ash
to separate ponds with once-through (nonrecycled) water, (2) the same
system with recycled transportation water, (3) direct sluicing of fly
ash and bottom ash to  temporary ponds, followed by excavation and truck-
ing of both to a common landfill, and (4) collection of bottom ash in
dewatering bins from which it is trucked  to a separate landfill and
collection of fly ash  in dry storage silos from which it is trucked to a
separate landfill.

     The fifth base case represents a situation in which the power plant
is burning a western-type coal which contains appreciable calcium,
making the ash subject to spontaneous cementitious reactions that affect
handling properties.  The handling and disposal system is designed to
forestall these reactions by keeping the  ash dry until shortly before
placement at the disposal site.
NEW PREMISES

     The FGD and waste disposal studies  that  are now in progress are
based on new design and economic premises.  During the 1977-1980 series
of studies it was recognized that changing  economic conditions,  fuel use
patterns, developments in.economic evaluation techniques,  and,  particu-
larly, developments in FGD technology and environmental legislation
justified revision of the TVA design and economic premises.   Consequently.
TVA began studies that led to the adoption  of new economic premises in
1979.  During this period numerous discussions were held with EPA,  EPRI,
and with other TVA organizations concerned  with the use of these premises.
                                    70

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Design Premises

     Essentially the same power plant conditions are retained.  For the
base case these are a new, midwestern, 500-MW, pulverized-coal-fired,
dry-bottom boiler.  The heat rate is increased from 9,000 to 9,500 Btu/kWh
and the excess air is increased from 33% to 39%, however.  The sulfur
content of the coal remains at 3.5% but the heating value is increased
from 10,500 to 11,700 Btu/lb.  The operating schedule is also changed to
5,500 hr/yr for 30 years.  A constant annual operating time is used to
facilitate levelizing of lifetim^ costs.

     Major changes were made in the FGD design premises to reflect
current regulations and to improve process reliabilities.  Required S0£
removal efficiency is now based on the 1979 NSPS.  For the base-case
coal these require an 89% removal efficiency instead of the 79% needed
to meet the 1971 NSPS used in the old premises.  In keeping with current
design trends a spare absorber train and provisions for emergency bypass
of 50% of the total flue gas are included.  The old premises contained
no spare absorber or bypass provisions.  In addition, ID booster fans,
instead of FD booster fans, are used in the new designs.  For nonrecovery
processes both pond and landfill waste disposal methods are revised to
reflect more recent environmental concerns.  These are primarily based
on RCRA Subtitle D (nonhazardous waste) guidelines and include provisions
for such factors as seepage and runoff control, security, monitoring,
and reclamation.

     FGD process design features are usually based on technology pre-
vailing at the time of the study.  The limestone scrubbing process is,
however, somewhat of a premise adjunct since it is used so frequently as
a basis of comparison in FGD studies.  This process serves as an example
of the changes in FGD technology that have occurred over the past few
years.  The current limestone process differs from the old process used
in the 1977-1980 studies in several respects.  A spray tower instead of
a mobile-bed absorber, forced oxidation to gypsum, and landfill waste
disposal are now included in the basic system.  The use. of a spray tower
results in a lower gas velocity of 10 ft/SBc instead of the 12.5 ft/sec
used in the old process with a mobile-bed absorber.

     The new limestone scrubbing process represents several industry
trends in limestone scrubbing that have become evident in recent years,
The use of a spray tower ^instead of more complicated mobile-bed and
venturi - spray scrubbers has become common.  The simpler spray tower is
expected to provide greater reliability and require less maintenance
although these: have not been, quantified in practice.  The problem of
waste disposal has also been addressed, both by increasing use of
stabilization, fixation, and landfill disposal techniques and by other
methods of producing a more tractable waste, such as oxidation to gypsum.

     The use of a spray tower, air oxidation, and landfill disposal in
the new process recognizes these trends.  The process is based in part
on continuing test work on spray towers, forced oxidation, and waste
                                     71

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dewatering at the EPA-spbhsored test facility at the Shawnee Steam
Plant.  Like the previous limestone scrubbing process, however, it is
generic and incorporates general industry information as well as data
from Shawnee.

Economic Premises

     Numerous changes were also made in the economic premises.  Specific
provisions for sales tax, freight, and overtime for construction delays
are included.  The method of calculating indirect capital investment is
simplified and modified to more accurately reflect complexity of engineering
and construction costs of processes evaluated.  Contingencies and allowances
for modification after startup are also defined as process-specific
variables reflecting degree of development and established technology.
Provision for recognition of anticipated royalties is also made.  Land
prices and interest during construction are increased.

     First-year revenue requirements are now calculated using levelized
capital charges (30-year life, capital recovery factor, 6% per year
inflation and 10% per year cost of money, discounted to the first year)
instead of the average capital charges used in the old premises.  In
addition, levelized lifetime revenue requirements are also calculated to
represent inflated and discounted costs over the life of the system.

     The base years for capital investment and first-year revenue require-
ments are also advanced to 1982 and 1984 respectively.  A project con-
struction period from 1981 to 1983 is now assumed, with plant startup in
early 1984.
COST COMPARISON OF OLD AND NEW PREMISES

     The key old and new design and economic premises for evaluation of
the limestone scrubbing process are shown in Table 5.  A stepwise cost
transition from the old premises and technology to those for the new
limestone scrubbing evaluation is shown in Table 6 and illustrated in
Figure 6.  Overall, the cumulative changes result in nearly doubled
capital investment and first-year revenue requirements.  The investment
increases resulting from the new economic premises are related to higher
indirect capital investment costs, particularly in interest during
construction, contractor expense, and working capital.  The increase in
first-year revenue requirements stems largely from capital charges based
on the capital investment.  New power plant coal and air rates, the
operating profile, and the 1979. NSPS all produce similar increases in
capital investment.  In these cases the main factors are increased flue
gas volume, increased lifetime.waste disposal requirements, and the more
stringent scrubbing conditions.   The effect on annual revenue require-
ments is similar except, of course, that the reduction in yearly operating
hours results in a reduction in costs.  Addition of reliability factors
(a spare scrubber train, emergency bypass, and a spare ball mill) also
cause appreciable increases in both capital investment and first-year
                                     72

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    TABLE 5.  COMPARISON OF OLD AND NEW PREMISE CONDITIONS

             USING THE LIMESTONE SCRUBBING PROCESS
                                   Old premises   New premises
Design Premises

Coal, Btu/lb
Excess air, %
Heat rate, Btu/kWh
Operating profile
  First year, hr/yr
  Lifetime, hr (30 years)
FGD
  SOX removal, %
  Emergency bypass, %
  Spare units
  Booster fan
Limestone process
  Absorber
    L/G, gal/kaft3
    Gas velocity, ft/sec
    AP, in. H20
  Forced oxidation
  Waste disposal
          10,500
              33
           9,000

           7,000
         127,000

       1971 NSPS
              0
              0
              FD

     Mobile bed
              50
           12.5
              8
              No
           Pond
      11,700
          39
       9,500

       5,500
     165,000

   1979 NSPS
          50
           1
          ID

 Spray tower
          90
        10.0
         1.4
         Yes
    Landfill
Economic Premises

Cost index year
  Capital investment
  Annual revenue requirements
Indirect capital costs
Land, $/acre
Interest during construction,
Limestone process contingency,
Pond contingency, %
Pond allowance for startup, %
Capital charges
Depreciation
            1979
            1980

           3,500
I              12
%             20
              20
               8
 Average  annual
   Straight line
        1982
        1984
     Revised
       5,000
        15.6
          10
          10
           0
   Levelized
Sinking fund
                               73

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TABLE 6.  COST COMPARISON IN TRANSITION FROM OLD TO NEW PREMISES




       AND TECHNOLOGY FOR THE LIMESTONE SCRUBBING PROCESS
Capital investment
Condition
Old premises and technology
Above with new economic
premises and pond
Above with new power plant
design premises
Above with new operating
profile
Above with 1979 NSPS
Above with reliability
factors (spares and bypass)
Above with spray tower
Above with landfill
Above with 1982, 1984 costs
k$
48,700

55,100

57,100

59,800
63,600

77,100
83,300
76,000
96,800
$/kW
98

110

114

120
127

154
167
152
194
% change
_

13

4

5
6

21
8
-9
28
% total change


13

17

23
29

58
71
56
99
First-year revenue requirements
k$
14,100

16,200

17,000

16,500
17,200

20,100
21,500
21,700
27,300
Mills/kWh
4.0

4.6

4.9

6.0
6.3

7.3
7.8
7.9
9.9
% change
_

15

5

-3
4

17
7
1
26
% total change
_

15

21

17
22

43
52
'54
94

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                                                             #
                                                            0°
    200-
     150-
H
Z
w  _
>  *
H
     100^
5!
      50-



      10-
o-
s
     .c
w



oo

H
fe

              SUM OF  PREMISE ft TECHNOLOGICAL CHANGES
                                            ^  ^
                      .".    C
                       Yfft
                                    //1
              SUM OF  PREMISE ft TECHNOLOGICAL CHANGES-
     Figure 6.   Stepwise conversion of  limestone scrubbing costs

                from old :to new premises  and technology.
                                 75

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revenue requirements,  The use of a spray tower instead of a mobile-bed
absorber increases costs primarily because of the lower flue gas velocity
and higher slurry recirculation rate, which requires larger ducting and
pumping requirements.

     Substitution of landfill for ponding substantially reduces capital
investment by eliminating pond construction costs.  The resulting reduction
in capital charges essentially counteracts the increased waste disposal
costs in first-year revenue requirements.

     The largest cost increase is a result of advancing the cost index
year from 1978 to 1982 for capital investment and from 1980 to 1984 for
first-year revenue requirements.

     Overall, economics in the form of inflation and higher interest
have the largest effect in comparison of the limestone process using the
old and new premises and technology.  Technical changes related to
improvements in reliability, such as bypass and redundancy provisions,
also have a large effect.  The higher SOX removal efficiency has less
effect than the economic and technical changes.
ADVANCED LIMESTONE SCRUBBING TECHNOLOGY

     As stated earlier, TVA is now conducting an. EPA-sponsored economic
evaluation of advanced limestone scrubbing technology.  The study encom-
passes recent developments in limestone scrubbing such as chemical
additives, increasing use of spray towers, forced oxidation, and landfill
techniques.  The complete results of this project will be published in
1981.

     Of particular interest at this time is the advanced limestone
system using a spray tower, forced oxidation, adipic acid addition and
landfill of the gypsum waste.  The interest comes from favorable results
at the Shawnee Test Facility.  Earlier bench- and pilot-scale studies
were made by TVA and EPA on adipic acid addition and EPA is sponsoring
an adipic acid demonstration unit at the Southwest Plant of Springfield
(Missouri) City Utilities.  The advantage of adipic acid (or other
similar additives) lies in its buffering action, which controls the
slurry pH at more favorable reaction conditions.  This increases the
reactivity of the slurry, improving S02 removal efficiency and increasing
limestone utilization.

     As a special feature, an economic comparison of the advanced process
with the new conventional and old conventional limestone processes is in
order.   The design conditions for the three processes are shown in
Table 7-

     Tables 8 and 9 show the capital investments and annual revenue
requirements for the three processes based on the base-case conditions
and the new premises that were discussed previously.  The cos'cs thus
                                    76

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            TABLE  7.  PROCESS DESIGN CONDITIONS AND PREMISES - LIMESTONE PROCESSES
Type of absorber
Forced oxidation
Adipic acid use
Waste disposal
Scrubber gas velocity,
 ft/sec
L/G, gal/kaft3
Limestone stoichiometry
Air stoichiometry
Percent sulfite oxidation
ID fan/FD fan
Spare scrubber
Filter cake solids, %
Pond settled solids, %
Spare ball mill
Reheat
Bypass available
                                 Advanced pro ces s
                                      New
                                  conventional
                                 Old
                            conventional
Spray tower
Yes
Yes (1000 ppm)
Thickener-filter-landfill

10
80
1.2
2.5
95
ID
Yes
80

Yes
In-line steam
50% emergency
Spray tower
Yes
No
Thickener-filter-landfill

10
90
1.3
2.5
95
ID
Yes
80

Yes
In-line steam
50% emergency
Mobile bed
No
No
Pond

12.5
58
1.3
0
30
ID
Yes

40
Yes
In-line steam
50% emergency

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    TABLE  8.  CONVENTIONAL AND ADVANCED LIMESTONE SCRUBBING PROCESSES

                           CAPITAL INVESTMENT

Direct Investment
Material handling
Feed preparation
Gas handling
S02 absorption
Reheat
Solids disposal
Total
Services, utilities, and miscellaneous
Total
Landfill or pond construction
Capital
Old
conventional3

3,498
3,485
9,600
19,830
2,851
2.063
41,327
2.480
43,807
.13,960
investment,
New
conventional"

3,497
3,484
11,129
22,988
3,304
2.868
47,270
2.836
50,106
2,076
500
k$
Advanced0

3,503
3,490
10,821
22,351
3,213
2,850
46,228
2,774
49,002
1,983
495
     Total
                                            57,767
               52,682
            51,480
Indirect Investment

Engineering design and supervision
Architect and engineering contractor
Construction expense
Contractor fees
Contingency

     Total fixed investment
 80,458
75,517
73,790
Other Capital Investment

Allowance for startup and modifications
Interest during construction
Land
Working capital

     Total capital investment

     $/kW
103,030
    206
Basis
  Upper Midwest plant location represents project beginning mid-1980, ending
  mid-1983.  Average cost baais, mid-1982.  Spare pumps, one spare scrubbing
  train, and one spare ball mill are included.  Disposal pond and landfill
  located 1 mile from plant.  Investment includes FGD feed plenum but
  excludes stack plenum and stack.

  a.  Old conventional process is a mobile bed absorber with onsite ponding
      of sulfite sludge.
  b.  New conventional process is a spray tower, forced oxidation and gypsum
      landfill.
  c.  Advanced system is same as b. but with adipic acid addition for
      enhanced S02 removal.
                                     78

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     TABLE  9.   CONVENTIONAL AND  ADVANCED  LIMESTONE  SCRUBBING PROCESSES

                         ANNUAL REVENUE  REQUIREMENTS
Annual cost, k$


Direct Costs - First-Year
Raw materials
Limestone
Adipic acid
Total raw materials cost
Conversion costs
Operating labor and supervision
FGD
Solids disposal
Utilities
Process water
Electricity
Steam
Fuel
Maintenance
Labor and material
Analyses
Total conversion costs
Total direct costs
Indirect Costs - First-Year
Overheads
Plant and administrative (60% of
conversion costs less utilities)
Total first-year operating and
maintenance costs
Levelized capital charges (14.7% of
total capital investment)
Total first-year annual revenue
requirements
Levelized first-year operating and
maintenance costs (1.886 x first-
year 0 and M)
Levelized capital charges (14.7% of
total capital Investment)
Levelized annual revenue
requirements

First-year annual revenue requirements
Levelized annual revenue requirements
Old
conventional


1,128
_
1,128


460
-

35
1,732
1,273
-

3,923
104
7,527
8,655



2.692

11,347

•15.145

26,492


21,401

15,145

36,545

9.63
13.29
New
conventional


1,128
-
1,128


658
529

26
2,018
1,365
199

4,025
104
8,924
10,052



3,057

13,109

14,234

27,343


24,724

14,234

38,958
Mills /kWh
9.94
14.17

Advanced


1,041
216
1,257


658
517

26
1,874
1,367
189

3,937
104
8,672
9,929



2,998

12,927

13,907

26,834


24,381

13,907

38,288

9.76
13.92

Basis
  Upper Midwest plant location, 1984 revenue requirements.
  New plant with 30-year life.
  Power unit on-stream time,  5,500 hr/yr.
  Coal burned, 1,116,500 tons/yr.
  Boiler heat rate,  9,500 Btu/kWh.
  Total capital investment:
    Old conventional - $103,030,000
    New conventional - $ 96,832,000
    Advanced           $ 94,608,000

                                    79

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incorporate a spare scrubber,  emergency bypass, and a 1981-1983, 1984
time period, among other differences from the FGD studies discussed
previously.  All of the costs  except those for landfill were developed
by the TVA Shawnee Computer Economics Program (15).

     Both the new conventional process and the advanced process have
slightly higher direct capital investment costs than the old conventional
process in most areas.  The old conventional process has disposal site
(pond) construction costs over ten times higher than the disposal site
(landfill) construction costs  than the others, however.  The result is a
slightly lower capital investment for the new conventional and advanced
processes.  The use of adipic  acid in the advanced process produces a
minor increase in material handling costs and much larger decreases in
absorber and disposal costs.  The increased reactivity of the limestone
slurry allows both less stringent scrubbing conditions and improved
limestone utilization, resulting in lower limestone consumption and less
unreacted limestone in the waste.

     In annual revenue requirements, the old conventional process has
lower conversion costs, primarily because of lower labor and supervision
and electricity costs, resulting in lower overall expense.   The increase
in labor and supervision cost  for the new conventional and advanced
processes is largely for disposal operations because trucking and earth-
moving operations are required.   In comparison of the new conventional
process and the advanced process, adipic acid addition causes a slight
overall reduction in costs, primarily because of lower limestone and
electricity consumption.
                                    80

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                               REFERENCES
1.  S.  V.  Tomlinson, F.  M. Kennedy, F.  A. Sudhoff, and R.  L. Torstrick.
    Definitive SOX Control Process Evaluations - Limestone, Double-
    Alkali, and Citrate FGD Processes.   TVA ECDP B-4, Tennessee Valley
    Authority, Office of Power, Emission Control Development Projects,
    Muscle Shoals, Alabama.  EPA-600/7-79-177, U.S. Environmental Protec-
    tion Agency, Office of Research and Development, Washington, D.C.,
    1979.

2.  K.  D.  Anderson, J. W. Barrier, W. E. O'Brien, and S. V. Tomlinson.
    Definitive SOX Control Process Evaluations:  Limestone, Lime, and
    Magnesia FGD Processes.  TVA ECDP B-7, Tennessee Valley Authority,
    Office of Power, Emission Control Development Projects, Muscle
    Shoals, Alabama.  EPA-600/7-80-001, U.S. Environmental Protection
    Agency, Office of Research and Development, Washington, D.C., 1980.

3.  J.  R.  Byrd, K. D. Anderson, S. V. Tomlinson, and R. L. Torstrick.
    Definitive SOX Control Process Evaluations:  Aqueous Carbonate,
    Wellman-Lord, Allied Chemical, and Resox® FGD Technologies.  Tennessee
    Valley Authority, Office of Power,  Division of Energy Demonstrations
    and Technology, Muscle Shoals, Alabama.  U.S. Environmental Protec-
    tion Agency, Office of Research and Development, Washington, D.C.
    (In press)

4.  G.  G.  McGlamery, R. L. Torstrick, J. W. Broadfoot, J. P. Simpson,
    L.  J.  Henson, S. V. Tomlinson, and J. F. Young.  Detailed Cost
    Estimates for Advanced Effluent Desulfurization Processes.  TVA
    Bulletin Y-90, Tennessee Valley Authority, Office of Agricultural
    and Chemical Development, Muscle Shoals, Alabama.  EPA-600/2-75-006,
    U.S. Environmental Protection Agency, Office of Research and Develop-
    ment,  Washington, D.C., 1975.

5.  J.  W.  Barrier, H. L. Faucett, and L. J. Henson.  Economics of
    Disposal of Lime-Limestone Scrubbing Wastes:  Untreated and
    Chemically Treated Wastes.  TVA Bulletin Y-123, Tennessee Valley
    Authority, National Fertilizer Development Center, Muscle Shoals,
    Alabama.  EPA-600/7-78-023a, U.S. Environmental Protection Agency,
    Office of Research and Development, Washington, D.C., 1978.

6.  J.  W.  Barrier, H. L. Faucett, and L. J. Henson.  Economics of
    Disposal of Lime/Limestone Scrubbing Wastes:  Sludge/Flyash Blending
    and Gypsum Systems.  TVA Bulletin Y-140, Tennessee Valley Authority,
    National Fertilizer Development Center, Muscle Shoals, Alabama.
    EPA-600/7-79-069, U.S. Environmental Protection Agency, Office of
    Research and Development, Washington, D.C. , 1979.
                                   81

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 7.   J.  D.  Veitch,  A.  E.  Steele,  and T.  W.  Tarkington.  Economics of
     Disposal of Lime/Limestone Scrubbing Wastes:   Surface Mine Disposal
     and Dravo Landfill Processes.   TVA EDT-105,  Tennessee Valley Authority,
     Office of Power,  Division of Energy Demonstrations and Technology,
     Muscle Shoals, Alabama.   EPA-600/7-80-022,  U.S.  Environmental Protec-
     tion Agency, Office of Research and Development, Washington, D.C. ,
     1980.

 8.   J.  I.  Bucy, J. L. Nevins, P- A. Corrigan,  and A. G. Melicks.  The
     Potential Abatement Production and Marketing of Byproduct Elemental
     Sulfur and Sulfuric Acid in the United States.  TVA S-469, Tennessee
     Valley Authority, Office of Agricultural and Chemical Development,
     Muscle Shoals, Alabama,  1976.

 9.   J.  I.  Bucy, R. L. Torstrick, W. L.  Anders,  J. L. Nevins, and P. A.
     Corrigan.  Potential Abatement Production and Marketing of Byproduct
     Sulfuric Acid in the U.S.  TVA Bulletin Y-122, Tennessee Valley
     Authority, Office of Agricultural and Chemical Development, Muscle
     Shoals, Alabama.   EPA-600/7-78-070, U.S. Environmental Protection
     Agency, Washington, D.C., 1978.

10.   W.  E.  O'Brien and W. L.  Anders.  Potential  Production and Marketing
     of FGD Byproduct Sulfur and Sulfuric Acid in the U.S. (1983 Projection).
     ECDP B-l, Tennessee Valley Authority,  Office of Power, Emission Control
     Development Projects, Muscle Shoals, Alabama  EPA-600/7-79-106, U.S.
     Environmental Protection Agency, Washington,  D.C., 1979.

11.   W.  L.  Anders.   Computerized FGD Byproduct Production and Marketing
     System:  Users Manual.  TVA ECDP B-2,  Tennessee Valley Authority,
     Office of Power,  Emission Control Development Projects,  Muscle Shoals,
     Alabama.  EPA-600/7-79-114,  U.S. Environmental Protection Agency,
     Washington, D.C., 1979.

12.   W.  E.  O'Brien, W. L. Anders, and J. D. Veitch.  Projection of 1985
     Market Potential for FGD Byproduct Sulfur and Sulfuric Acid in the
     U.S.  TVA EDT-115, Tennessee Valley Authority, Office of Power,
     Division of Energy Demonstrations and Technology, Muscle Shoals,
     Alabama.  EPA-600/7-80-131,  U.S. Environmental Protection Agency,
     Washington, D.C., 1980.

13.   T.  A.  Burnett  and W. E.  O'Brien.  Preliminary Economic Analysis of
     a Lime Spray Dryer FGD System.  TVA EDT-112,  Tennessee Valley
     Authority, Office of Power,  Division of Energy Demonstrations and
     Technology, Muscle Shoals, Alabama.  EPA-600/7-80-050, U.S. Environ-
     mental Protection Agency, Washington,  D.C.,  1980.

14.   T.  A.  Burnett  and K. D.  Anderson.  Technical Review and Economic
     Evaluation of  Spray Dryer FGD Systems.  Tennessee Valley Authority,
     Office of Power,  Division of Energy Demonstrations and Technology,
     Muscle Shoals, Alabama.   U.S.  Environmental Protection Agency,
     Washington, D.C.   (In press)
                                    82

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15.   C.  D.  Stephenson and R.  L.  Torstrick.   Shawnee Lime/Limestone
     Scrubbing Computerized Design/Cost-Estimate Model Users Manual.
     ECDP B-3, Tennessee Valley Authority,  Office of Power, Emission
     Control Development Projects, Muscle Shoals, Alabama.   EPA-
     600/7-79-210, U.S.  Environmental Protection Agency, Washington,
     D.C.,  1979.
                                    83

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          S02 AND NOx ABATEMENT FOR COAL-FIRED BOILERS IN JAPAN
Jumpei Ando

Faculty of Science and Engineering, Chuo University
Kasuga, Bunkyo-ku, Tokyo 112
     The total capacity of coal-fired utility boilers in Japan,
which was only 4,300 MW (3.7% of total utility power) in 1979, is
expected to increase to 10,000 MW (5.6%) in 1885 and to 22,000 MW
(10.0%) in 1990.  Most of the boilers will apply FGD by the wet
limestone-gypsum process because of its reliability and relatively
low cost.  To save energy and water, F.GD systems with a low
pressure drop and small water consumption are preferred.  Tests on
FGD by a dry carbon process are under way.

     NOx concentrations in flue gases from existing coal-fired boilers
have been lowered to 200 - 350 ppm by combustion modification including
staged combustion and the use of low-NOx burners.  For further abatement,
selective catalytic reduction (SCR) has started to be applied to several
coal-fired boilers.  The first full-scale combination system of SCR
and FGD was put into operation in April 1980.  The plant cost for
SCR is about one-third that for FGD.  A new combustion technology has
also been developed in attempts to lower NOx below 100 ppm.
  Preceding page blank
                                  85

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               1.  COAL USAGE AND POLLUTION CONTROL IN JAPAN
     Most utility power companies in Japan switched fuel from coal to
oil between 1960 and 1974 except Electric Power Development Co. (EPDC)
which was established by the Japanese government jointly with major
power companies to use domestic coal.  Due to the recent rise in oil
and gas prices, power companies have started to construct new coal-fired
boilers (Table 1), most of which will use imported coal because the
supply of domestic coal is limited to 20 million tons yearly.  Although
Japan has imported over 60 million tons of coal yearly, all of the
imported coal has been for coke production for the steel industry.  The
import of fuel coal has been started and is expected to reach 45 million
tons in 1990.

     Major problems with coal usage are (1) emissions of SO,,, NOx and
particulates on combustion, (2) handling and storage problems, and (3)
ash disposal.  Those problems are serious in Japan where a large
population is concentrated in a small land space.  The new boilers
are to be located in regions relatively far from large cities and
industrial districts, where the environmental regulations by the Central
Government are not quite stringent.  However, in order to construct
a large plant, it is necessary to make an agreement with local governments,
by which extensive countermeasures for pollution control are necessitated.

     All of the new coal-fired boilers will need FGD.  NOx concentrations
in flue gas from major coal-fired boilers has been reduced to 200 -
350 ppm while the emission standard by the Central Government is
400 ppm for new boilers and 480 ppm for existing ones.  Further reduction
will be needed for new boilers.  Some power companies have started to
apply selective catalytic reduction (SCR) which usually removes about
80% of NOx (Table 1).

     A new combustion technology to lower NOx concentration below
100 ppm with coal and below 50 ppm with oil has been developed.
(Section 6.2).

     Particulates can be removed sufficiently by a combination of
electrostatic precipitator and wet FGD.  A bag house has been tested
but has not been considered promising for a large boiler.

     In attempts to solve the coal handling problem, coal-oil mixture
(COM)  has been studied extensively and may be used for some of the new
boilers.   The major drawback with COM is that more than half of the
energy is derived from oil.  To save oil, coarse-grain COM has been
tested,  which uses up to 6 mm grains of coal which is transported with
oil as a slurry and separated from oil for burning.

     The largest problem with coal usage may be ash disposal, because
landspace for discarding is limited.  New uses of the ash, as feedstock


                                  86

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               Table 1  Coal-fired utility boilers  in Japan

                            (Larger than  175 MW)
                                                     Year  of  Completion
Power
company
EPDC

it

it

ii

ii

ii
Chugoku
ii
Hokkaido
ti
Kyushu

ii

Joban Kyodo

Tohoku

Tokyo

Power
station
Isogo

Takasago

Takehara

Matsushima

Matsuura

Mito
Shimonoseki
Misumi
Tomato-Atsuma
Sunagawa
Matsuura

Reihoku

Nakoso

Noshiro

Mito

Boiler
No.
1
2
1
2
1
3
1
2
1
2
1
1
1
1
4
1
2
1
2
8
9
1
2
1
2
Capacity
MW
^265
265
250
250
250
700
500
500
1,000
1,000
1,000
175
700
350
125
700
700
700
700
600
600
600
600
1,000
1,000
a
Boiler FGD SCR
1967 1976
1969 1976
1968 1975
1969 1976
1967 1977 1981
1982 1982 1982
1981 1981
1981 1981
1984b
1986b
1988b
1967 1979 1980
1985b
1980 1980 1980°
1982 1982
1984b
1988b
1987b
1989b
1983d 1983
1983d 1983
1985b
1985b
1988b
1988b
a  Selective catalytic reduction of NOx
b  Planned.
c  Treating  one-fourth of the gas.
d  Mostly oil will be used with less coal for a while without FGD.
                                      87

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for cement production replacing clay, as filler for asphalt, as raw
material for aggregate,  etc.,  have been developed.

     Studies have been carried out also on fluidized bed combustion
(FBC), gasification, and liquefaction of coal, but not as extensively
as in the USA.  The major problem with FBC in Japan is the difficulty
in disposing of the ash containing lime and calcium sulfate.  Tests
have been conducted in search  for an S02 absorbent that can be separated
from ash, regenerated and recycled, but so far do not seem promising.
Gasification and liquefaction   may not be suitable to Japan which has
to depend on imported coal,  since a considerable portion of energy
of coal is consumed by gasification or liquefaction.  Although
liquefaction may be important  in future, the plant may have to be
constructed abroad and the product imported.
            2.  STATUS OF FGD FOR COAL-FIRED UTILITY BOILERS
     Before 1979, FGD plants for coal-fired utility boilers were limited
to the 5 plants of EPDC.   Among the EPDC plants,  two at Takasago Station
had an appreciable scaling problem until 1977 mainly at the mist
eliminator which had been washed with a circulating liquor saturated
with gypsum.1)   By using  fresh water together with the liquor for the
wash, the scaling problem was solved.!»2)   Since  1978, all of EPDC's
FGD plants have been operated with virtually 100% operability and
reliability (Table 2).

        Table 2  Operation hours of EPDC's boilers and FGD plants
                     (April 1978 through March 1979)

                                  Operation hours

                 Boiler        Boiler (A)*   FGD  (B)   B/A (%)
Isogo

Takasago

Takehara
No.
No.
No.
No.
No.
1
2
1
2
1
7,705
8,206
7,829
8,167
7,583
7,705
8,206
7,823
8,147
7,580
100.0
100.0
99.92
99.75
99.95
             *   When an  FGD plant  is shut down due to its own trouble,
                the  boiler is  operated by using low-sulfur oil.
                Therefore,  B/A (%)  shows operability as well as
                reliability.
                                 88

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     Operation parameters of the plants are shown in Table 3.  Although
the plants are highly reliable and removes over 90% of 862 and over
70% of fly ash, they have the following drawbacks:  (1) A large gas
pressure drop due to the use of a venturi or perforated plate scrubber
to attain a high dust removal efficiency, which results in a large
power consumption.  (2) Requirement of a large amount of water for gas
cooling and also for purging wastewater from the system in order to
maintain chlorine in the scrubber liquor below a certain level for
corrosion prevention.  (Usually more than half of the water charged
to the FGD system is volatilized in the prescrubber).

     In order to lower the pressure drop, new FGD plants, including
Chugoku Electric's Shimonoseki plant constructed by MHI and two
EPDC plants at Matsushima under construction by Babcock Hitachi and
IHI, use a spray tower for gas cooling and particulate removal.  A gas-
gas heater (heat exchanger) is used for the new plants as well as the
Tomato-Atsuma plant of Hokkaido Electric in order to cool the FGD inlet
gas to save water and to heat the FGD outlet for energy conservation.

     Dry processes for FGD have received attention as a possible way
for further improvement and also because of the convenience for use
in conjunction with selective catalytic reduction of NOx.  An activated
carbon process has been tested at EPDC's Takehara station.   (Section 6.1)
The Electric Power Industry Federation also is to make pilot plant
tests on activated carbon processes for coal-fired boilers at 3 power
stations.
            3.  NOx ABATEMENT AND COMBINATION OF SCR AND FGD
3.1  NOx Regulation and Selective Catalytic Reduction (SCR)

     NOx concentration in flue gases from coal-fired boilers has been
restricted by the emission standards by the central government to a
level below 480 ppm for existing boilers and below 400 ppm for new
boilers.  The concentration can be achieved by combustion modification
without appreciable difficulty.  Most local governments, however,
enforce much more stringent regulations.  For example, Yokohama City,
in an effort to lower the ambient N02 concentration from the current
0.06 - 0.07 ppm in daily average to 0.04 ppm, has asked EPDC's Isogo
Station to lower to 169 ppm the NOx concentration in flue gases from
the existing two 265 MW coal-fired boilers.  EPDC has lowered the
NOx concentration to 200 ppm by combustion modification including
staged combustion and low-NOx burner and has been making further efforts
to meet the requirement.  Isogo Station has a limited landspace in
which they managed to retrofit FGD plants and has no more space to
install a flue gas treatment (FGT) plant for NOx removal.  Therefore,
                                  89

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                   Table  3  Operation parameters of FGD plants for coal-fired utility boilers
Power company
Station
Boiler No.
Boiler capacity (MW)
FGD constructor
FGD start-up
Gas treated (1,000 Nm3/hr)
Inlet S02 (ppm)
Inlet dust (mg/Nm3)
Prescrubber (cooler)
Type
L/G (liters/Nm3)
Scrubber (S02 absorber)
, Type
L/G
Outlet S02 (ppm)
Outlet dust (mg/Nm3)
S02 removal efficiency (%)
Dust removal efficiency (%)
Pressure drop (mm I^O)
Wastewater (t/hr)
Energy requirement (%)n
Reliability (%)*
EPDC
Isogo
1
265
IHla
May '76
821
450
1,500
EPDC
Takasago
1
250
Mitsuib
Feb. '75
792
1,500
100
EPDC
Takehara
1
250
BHC
Feb. '77
793
1,730
400

Venturi
7
Venturi
6
Venturi
2.5

Venturi
7
25
50
94.4
96.6
360f
10
2.9
100.0
Venturi
6
100
30
93.3
70.0
325f
7.5
3.2
99.9
ppe
7
100
50
94.2
87.5
615f
12
3.3
100.0
EPDC
Matsushima
1
500
IHIa
Jan. '81
1,826
1,000
300
2
500
BHC
Jan. '81
1,826
1,000
300

Spray
Spray
2.8

Spray
13.4
50
30
95.0
90.0
Spray
15
50
30
95.0
90.0
133§



Chugoku
Shimonoseki
1
175
MHId
July '79
586
1,310
830

Spray
3

Packed
14
55
50
95.8
94.0
120f
15
2.1
100.0
Hokkaido
Tomato
1
350
BHC
Oct. '80
1,268
232
45

Venturi


PPe

23

90.0





a  Ishikawajima-Harima Heavy Industries
c  Babcock Hitachi K.K.
f  By two scrubbers and mist eliminators
h  Percent of power generated
b  Mitsui Miike Machinery Co.
d  Mitsubishi Heavy Industries      e  Perforated plate
g  By two scrubbers
i  EGD operation hours percent of desired FGD operation hours

-------
they need to reduce NOx further by improved combustion.  Even more
stringent regulations may be applied for new larger boilers, necessitating
FGT.

     Among many ways of FGT developed in Japan, selective catalytic
reduction (SCR) that uses ammonia and catalyst at 300 - 400°C is by
far the most advanced method, which has been used in constructing
about 100 commercial plants mainly for flue gas from oil-fired boilers.
The advantages of SCR over other FGT processes are simplicity and
reliability which enable unattended operation, lack of the by-product
disposal problem, and relatively low cost.  SCR is conveniently applied
to flue gas leaving a boiler economizer at 300 - 400°C.  The major
reaction is shown below:

     4NO + 4NH3 + 02 = 4N2 + 6H20

     At the early stage of development, SCR encountered the following
technical problems, most of which have been solved by recent improvements:
(1) Catalyst poisoning by SOx in flue gas.  (2) Catalyst pluggage
by dust.  (3) Catalytic oxidation of a portion of S02 to S03.   (4) Leak
ammonia from SCR reactor, which reacts with 863 and H20 to form
ammonium bisulfate deposit in an air preheater.

     Many of the catalysts developed recently are based on Ti02 with
small amounts of V20^ and other components, are resistant to SOx,
and oxidize about 1% or less S02.  In order to prevent dust plugging
of the catalyst, parallel flow type reactors with honeycomb, plate,
and tube catalysts have been used for dusty gases such as coal-fired
boiler flue gas.

     More than 90% of NOx can be removed by using over 1 mol NH3 to
1 mol NOx as shown in Figure 1.  However, 80% removal has been  generally
applied to utility boilers as the optimum control level, because
compared with 90% removal, it requires about 40% less catalyst  resulting
in the reduction of cost as well as pressure drop and also because
it can reduce leak ammonia to a low level (5 ppm or below) to minimize
the deposit of ammonium bisulfate in the air preheater.  Over 90%
removal with a low leak NH3 is difficult for a large boiler because
.the gas velocity as well as NOx concentration is not uniform in different
parts of the duct.

     Low-temperature catalysts active at 150 - 250°C have also  been
developed but have not been used commercially yet because ammonium
bisulfate forms on the catalyst and lowers its activity.  Ammonium
bisulfate can be removed by heating the catalyst to over 350°C.  The
low-temperature catalyst may not be suitable for boilers for which
economizer outlet gas around 350°C can be treated but may be useful
for other sources for which only cold gas around 200°C is available.
                                  91

-------
      g
      0)
      t-i
         100
          90
          80
          70
          60
                            20
                               _L
                                                             10
                                                                  e
                                                                  a
                                                                  a.
                                                                  cd
                                                                  0)
                                                                  1-1
          0.6
0.7
0.8       0.9


   mole ratio
                                                 1.0
                          1.1
 Figure 1  Performance of honeycomb  catalyst for coal-fired boiler


           flue gas  ( Inlet NOx  300  ppm,  at  370 °C.   SV means space


           velocity: flue gas volume per  hour divided by catalyst


           volume.  For high-dust system)
  High-dust system
B
320-400
/
SCR
320-400
s
APR
150-160
V
/
ESP
150-160
	 ^
FGD
 Low—dust system
B
320-400

Hot
ESP
320-400

SCR
320-400
	 ?
APH
150-160
/
FGD
Figure 2  Systems for coal-fired boiler flue gas treatent (Figures show
      gas temperature, °C.
B: Boiler   APH: Air preheater)
                               92

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3.2  Combination of SCR and FGD

     At an early stage of development, the SCR reactor was placed
downstream of FGD in order to reduce SOx poisoning and dust plugging.
This system, however, requires a large amount of energy for heating
the gas after FGD and has not been used since SOx-resistant parallel
flow type catalysts have been developed.  Figure 2 shows two combination
SCR/FGD systems currently used for coal-fired boilers.  In both
systems, the economizer outlet gas at 330 - 400°C is treated by SCR,
cooled to 150°C by an air preheater, and then subjected to FGD.  The
high dust system treats the gas with full dust load (15 - 25 grams/Nm3)
by SCR, and therefore the catalyst should be hard in order to avoid
erosion by dust and thus is less porous and may not be highly
active.  On the other hand, the low dust system uses a hot electrostatic
precipitator (ESP) upstream of SCR, which is suitable for dust removal in
flue gas from low-sulfur coal.  The hot ESP usually reduces the dust
to 100 - 200 mg/Nm3 and protects the catalyst from erosion.  However,
the dust leaving the hot ESP is finer and richer in alkaline components
and tends to deposit on the catalyst surface.  The problem of ammonium
bisulfate deposit in the air preheater is also appreciable with the
low dust system while it is insignificant with the high dust system
(Section 5.3).  Therefore, leak ammonia should be kept at a lower level
with the low dust system than with the high dust system.

     As shown in Table 4, the Shimonoseki plant, Chugoku Electric
uses the high dust system while the Tomato-Atsuma plant of Hokkaido
Electric and the plants at Takehara, EPDC use the low-dust system.
Two plants at Nakoso, Joban Joint Electric will use the high dust system.

           Table 4  SCR plants for coal-fired utility boilers
Company
Chugoku
Hokkaido
EPDC

EPDC
Joban

Station
Shimonoseki
Tomato-Atsuma
Takehara

Takehara
Nakoso

Capacity
(MW)
175
350 x 1/4
250 x 1/2
250 x 1/2
700
600
600
Vendor
MHI
BH
BH
KHIa
ndb
MHI
IHI
bUK
Dust
High
Low
Low
Low
Low
High
High
type
Catalyst
Honeycomb
Plate
Plate
Tube
,b
nd
Honeycomb
Honeycomb
Comp-
letion
1980
1980
1981
1981
1982
1983
1983
     a  Kawasaki Heavy Industries
b  Not decided
                                  93

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     The flue gas leaving the SCR reactor contains a small amount of
ammonia, which is caught by a prescrubber of the FGD system.  Although
ammonia has no adverse effect either on the operation of wet lime/
limestone process FGD or on the quality of by-product gypsum, it is
contained in a small amount in wastewater from the FGD system.  If
needed, the ammonia in the wastewater can be removed by a conventional
biochemical treatment (activated sludge process) or by ammonia stripping.
The latter has been used at the Owase plant, Chubu Electric while the
former is to be used at the Takehara plant, EPDC.
3.3  SCR Cost

     Examples of SCR plant cost for utility boilers are shown in
Table 5.  The cost for the new gas-fired boiler at Chita was 1,860
yen/kW, while that for the new oil-fired boiler at Kudamatsu was
2,860 yen/kW.  Those for existing oil-fired boilers at Kudamatsu and
Chita were considerably higher than that for the new oil-fired boiler,
because of complicated duct work for retrofitting (Kudamatsu and Chita)
and the requirement of additional fans (Kudamatsu).  The SCR plant for
coal at Shimonoseki is more costly than for oil.

     The difference in cost with the fuel type is due mainly to the
amount of catalyst needed.  Generally speaking, an active pellet
catalyst can be used for clean gas, while for flue gas from oil
containing 20 - 100 mg/Nm3 of dust, a honeycomb catalyst with a
channel size of 6 - 7 mm and wall thickness of 1 - 1.5 mm consisting of
SOx resistant material has been used in a volume 3-4 times that of
the pellet catalyst.  For coal, the catalyst volume may be nearly
double that for oil because of a larger channel size of honeycomb for
dust plugging prevention and a harder structure for erosion prevention
resulting in lower activity.

     Estimated SCR costs for new 700 MW utility boilers using coal and
low-sulfur oil are shown in Table 6.  Honeycomb catalyst is used for
both oil and coal.  The assumed channel size and wall thickness in
millimeters are 6.6 and 1.4 for oil, 7.4 and 1.6 for coal with the
low-dust system, and 8.2 and 1.8 for coal with the high-dust system.
Leak ammonia is maintained below 10 ppm for oil (low sulfur) and coal
with the high dust system while it is kept below 5 ppm for coal with
the low-dust system which is liable to air  preheater  plugging.  Based
on those assumptions, an equal space velocity was assumed for high and
low dust systems of coal.  The space velocity is about one-half that
for oil.

     The investment cost including civil engineering and test operation
for 80% NOx removal is nearly 4,000 yen/kW for oil and nearly 7,000
yen/kW for coal, while the cost for 90% removal is higher by about 30%
for oil and 40% for coal.  The annualized SCR costs in yen/kWhr for
80% removal,  assuming 7 years' depreciation, 70% boiler utilization,
                                  94

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                       Table  5   Cost of SCR plants for utility boilers (in battery limits)
                                                     NOx
Space  .  Plant cost   Year
in
Power
company
Chubu
Chubu
Chugoku
Chugoku
Chugoku
Power
station
Chita
Chita
Kudamatsu
Kudamatsu
Shimonoseki
Boiler
(MW)
700
700
375
700
175
Fuel
Gas
Oilb
Oilb
oiib
Coal
New or
retrofit
New
Retrofit
Retrofit
New
Retrofit
removal
(%)
Over 80
Over 80
Over 80
Over 80
Over 50°
Const-
ructor
BH
MHI
IHI
IHI
MHI
Catalyst
type
Pellet
Honeycomb
Honeycomb
Honeycomb
Honeycomb
velocity
(hr-1)
20,000
6,000
5,500
5,500
3,000
i 	
I09yen
1.3
2.2
2.2
2.0
1.7d
yen
kW
1,860
3,570
5,870
2,860
9,710d
com-
plete<
1977
1980
1979
1979
1980
      a  Flue gas volume per hour divided by catalyst volume
      b  Low-sulfur  oil
      c  Catalyst for  50% removal has been used to meet the current regulation, while the SCR system has been
         designed for  80% removal.
      d  Including boiler modification for economizer bypass.

-------
      Table 6  Estimated SCR cost for new 700 MW utility boilers

                Annual power generation 4,292,400 MWhr.   70% utilization.
                LeakNH3:   5-10 ppm for oil and coal with high-dust
                system.   Less than 5 ppm for coal with low-dust system

                                                             Coal
Fuel                                 Oil (low S)     (high and low dust)
Flue gas, Nm3/hr. (NOx ppm)
NOx removal efficiency (%)
Space velocity (hr )
Investment cost
Q
Catalyst (billions of yen)
Other ( " )b
Total ( " )b
Total (1,000 yen/kW)
Annual cost (billions of yen)
Capital cost
Catalyst
Other6
Total
Annualized cost (yen/kWhr)
(1,000 yen/Nm3 of NOx removed)
2,000,000
80
5,100

1.22
1.50
2.72
3.89

0.50
0.61
0.27
1.38
0.32
1.15
(120)
90
3,400

1.82
1.75
3.63
5.10

0.62
0.91
0.31
1.84
0.43
1.39
2,300,000
80
2,700

2.81
2.00
4.81
6.87

0.78
2.81
0.48
4.07
0.95
1.20
(300)
90
1,700

4.46
2.30
6.76
9.66

1.02
4.46
0.55
6.03
1.40
1.58
                    3                           3
a  3.1 million yen/m  for oil,  3.3 million yen/m  for coal.

b  Including civil engineering  and test operation.

c  Interest (10%)  on initial charge of catalyst and interest and depreciation
   (25%) on investment cost excluding catalyst.

d  Catalyst life:   2 years for  oil and 1 year for coal.
e  Ammonia, power, etc.
                                  96

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and a catalyst life of 2 years for oil and 1 year for coal, are 0.32
for oil and 0.95 for coal, while the costs per unit amount of NOx
removed is just about equal for oil and coal.  Compared with 80%
removal, 90% removal costs about 40% more iri yen/kWhr.  Actually
90% NOx removal may be difficult for a large boiler without increasing
leak NH3, because gas velocity as well as NOx concentration may not
be uniform in different parts of the SCR reactor inlet.

     For coal, about 70% of the annualized SCR costs is accounted
for by catalyst.  If the catalyst is useful fpr 2 years, the costs
will be lowered by about 35%.  The catalyst life is usually guaranteed
for 1 year for both oil and coal.  Operation experiences have shown
that the catalyst for oil may be useful for over 3  years.  It may be
possible to extend catalyst life for coal to 2 years,
                 4.  SHIMONOSEKI PLANT, CHUGOKU ELECTRIC
4.1  Outline
     Shimonoseki Station of the Chugoku Electric Power Co. has two
boilers — a 175 MW coal-fired boiler (No. 1) and a 400 MW oil-fired
boiler (No. 2).  Regulations for the station are shown in the following
table.

              Table 7  Regulations for Shimonoseki Station

Air pollution control

   k Value                    2.7 (Ground level concentration 0.0047 ppm)

   SOx (total)                Below 412 Nm3/hr

   Particulates               Below 130 kg/hr
     No. 1 Boiler             Below 200 mg/Nm3

     No. 2 Boiler             Below  40 mg/Nm3
   NOx                        Below 330 Nm3/hr

     No. 1 Boiler             Below 350 ppm

     No. 2 Boiler             Below 170 ppm
   Floating particulates      Below 0.2 mg/Nm3
                                  97

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Water pollution control

   pH                         5.8 - 8.6

   Suspended solids         | Below 12 kg/day

                            '  Below 15 mg/liter

   Normal-hexane-soluble
material
Chemical oxygen demand
J Below 0.8 kg/day
» Below 1 mg/liter
( Below 12 kg/day
\ Below 15 mg/liter
     The No. 1 boiler was completed in 1967 and was burning coal and
oil in the ratio of 25 to 75 before a full scale FGD plant was completed
in July 1979 using the MHI wet limestone-gypsum process.  After the
FGD plant was put into operation, coal and oil was used in the ratio
of 50 to 50.  It was difficult to use larger amounts of coal because
of the NOx regulation (below 350 ppm) .  Although the regulation may be
met by combustion modification even with the burning of coal only, it
was likely that further NOx reduction might be required in future.
Chugoku Electric, therefore, decided to install a full-scale SCR unit,
which was completed in March 1980 to allow combustion of coal only.
The SCR unit is the first full-scale plant for a coal-fired boiler
in the world and has the nature of a demonstration plant.

     Figure 3 shows the combined system of SCR and FGD for the No. 1
boiler.  The flue gas is first subjected to SCR at 330 - 400°C, passed
through two trains of air preheaters and dust collectors (multicyclone
and ESP), and then undergoes FGD after it is passed through a heat
exchanger.

     The No. 2 boiler is a relatively new one and has used a high-sulfur
oil with FGD by the MHI wet limestone-gypsum process.


4.2  SCR System

     The design basis of the SCR system is shown below:

        Boiler capacity         175 MW

        Fuel                    Coal

        Gas flow rate           550,000 Nm3/hr

        Gas temperature         370°C

        Inlet NOx               500 ppm

        Outlet NOx              250 ppm (100 ppm in future)


                                  98

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                  Boiler
ID
                                                                                                 Stack
                                                                                                Heat exchanger
                                                                                                (Gas-gas heater)
                                    SCR  «  Selective  catalytic reduction of NOx
MC : Multicyclone
                         Figure  3   Flue  gas  treatment  system for No.l  coal-fired boiler  (175 MW)

                                  (Shimonoseki  Power Station,  Chugoku  Electric)

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        NOx removal efficiency    50% (80% in future)

        Inlet SOx                 1,600 ppm
        Reactor                   One reactor, with downflow of gas

        Catalyst                  Honeycomb.   Square type with 10 mm
                                  pitch (about 8.2 mm opening)

        Space velocity            3,000 hr"1
     The No. 1 boiler is for base load and the gas temperature at
economizer outlet is normally around 360°C,  suitable for SCR.  The
load is occasionally lowered to 25% of full  load, resulting in the drop
of the gas temperature to 300°C.   Since ammonium bisulfate may deposit
on the SCR catalyst during the low-load operation, a bypass system was
installed as shown in Figure 3 to control the gas flow by dampers
to mix a portion of hot gas with the economizer outlet gas to maintain
the gas temperature.

     An SCR reactor was installed beside the boiler so that the treated
gas is sent to the existing air preheaters.   The reactor contains
5 horizontal layers of honeycomb catalyst, through which flue gas is
passed downwards.  The flue gas contains about 410 ppm NOx, 360 ppm
SO^ and nearly 20 grams/Nm3 of fly ash.  A layer of "dummy" spacer
with the same shape as the honeycomb was placed on top of the first
honeycomb layer, in order to maintain a uniform parallel gas flow and
to prevent catalyst erosion by fly ash.

     Planning and design of the SCR system was started in July 1979.
Construction was begun in October 1979.  Boiler modification and
reactor connection were performed during the shutdown of the boiler
for annual maintenance between February 1 and March 31, 1980.  Since
start-up of operation in April 1980, the boiler, the SCR system and
the FGD system have been operated without trouble.

     Current regulations require about 50% NOx removal.  Therefore,
a NH3/NOx mole ratio of about 0.56 has been used to reduce NOx
concentrations from 410 to 185 ppm (55% removal) and to maintain leak
NH3 at reactor outlet below 3 ppm.  In future, 80% of NOx may be
removed by increasing the amount of catalyst and by using about 0.82 mol
NH3 to 1 mol NOx, keeping leak NH3 below 5 ppm.

     A catalyst life of 1 year is guaranteed by MHI, which will take
all of the spent catalyst when fresh catalyst is placed.  Replacement
of catalyst will require 15 days with 15 workers working 7 hours a day.

     The air preheater has had a soot blow system on the cold side which
has been operated 4 times a day,  two hours each time.  When the SCR
system was installed, an additional soot blow system was installed on
the hot side of the preheater, which has also been operated 4 times
                                  100

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a day, 2 hours each time.  The plugging problem of the preheater by
ammonium bisulfate has thus been prevented. The soot blow system will
be used less frequently.
     The total investment cost was about 2 billion yen including the
boiler modification of which 1.7 billion was paid to the constructor.
4.3  FGD System

     A flow sheet of the FGD system is shown in Figure 4.  Flue gas
leaving the air preheater at 160°C is cooled to about 95°c by a
Ljungstrom type heat exchanger and introduced into a semiventuri type
spray scrubber newly developed by MHI for particulate removal, and
then into a grid packed tower with a holding tank at the bottom and
a mist eliminator at the top.  Limestone slurry is fed to the tank.
The treated gas at 55°C is heated to 120°C by the heat exchanger
eliminating gas heating by oil firing.  About 90% of both S02 and
particulates are removed (Tables 3 and 5).  Slurry handling systems —
oxidation of calcium sulfite, gypsum centrifuge, etc., are similar to
those of the standard MHI process.2)

     After its startup  in July 1979, the FGD plant was operated
continuously without trouble until February 1980, when the boiler was
shut down for annual maintenance.  During the operation period, coal
and oil were used in the ratio of 25 to 75 at the beginning and then
in the ratio of 50 to 50.  Fresh water, at the rate of 30 tons/hr?
was fed mainly to the syray tower and used partly for mist eliminator
wash.  Of the 30 tons/hr, 13 tons were volatilized, 2 tons went into
gypsum as water of crystallization and moisture, and 15 tons were
sent to a wastewater treatment system.

     Inspection during the shutdown period detected a little deposit
of particulates in the heat exchanger and a slight erosion of rubber
lining but neither scaling nor corrosion.  The soot blow system was
reinforced during the shutdown period in order to eliminate the deposit
formation in the heat exchanger.

     Since its restart in April, using coal only this time, the FGD
system has been operated trouble-free again.  Because a fan is placed
upstream of the heat exchanger, a small amount of inlet gas at 160°C
leaks in the heat exchanger to mix with the FGD outlet gas, thus
lowering the removal efficiency of SO? and particulates to some extent
(Table 8).  Placing the fan between the heat exchanger and the
prescrubber (co.oler) results in the leak of the FGD outlet gas to  the
inlet and an increase in removal efficiency, but it may cause corrosion
of the fan due to condensation of sulfuric acid at low temperatures
around 90°C.  MHI has been testing a new type of air preheater without
gas leakage.
                                  101

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                Fan
               o
                                                                      Stack
     l"i
VvV
Dust
collector
160°C

 Fan
r-
  120°C
                  Heat
                  exchanger

                  (Gas-gas
                    heater)
                Water
                (22t/hr)
                                              Water
                        I(St/hr)
                                                Mist
                                                eliminator
  Wastewater(10t/hr)
       Limestone
                         ^-^ to_ scrubber
                                     l
                                                                        Oxidizer
                                                                Air
                                                            rQ
                       Cooler
                  Scrubber
   Wastewater(5t/hr)

T


Thick-
ener
f

	 ^r-
£


/
*-i" >
Centr
                                                          Tank     (j
                                                                                                    n
           Figure 4  Flowsheet of FGT) system for No.l boiler at- Shimonoseki Power Station

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   Table 8  862 and particulate removal efficiency(Shimonoseki plant)

             Concentration and          Coal and oil      Coal only
Pollutants      removal efficiency       (50 ; 50)    Low S    Medium S

S02          FGD inlet (ppm)              1,230         355     1,310
             FGD outlet (ppm)                78          20        55

               Removal efficiency(%)         93.7        94.4      95.8
             HEaoutlet (ppm)                136          38       115

               Removal efficiency(%)         89.0        89.2      91.2

Particulates  FGD inlet (mg/Nm3)            200        1280       830

              FGD outlet(mg/Nm3)             12          80        50
                Removal efficiency(%)        94.0        93.8      94.0

              HEa outlet (mg/Nm3)            21         130        85

                Removal efficiency(%)        89.5        89.8      89.7
   a  Heat exchanger

     Ammonia contained in a small amount in flue gas has had no adverse
effects on FGD and on the quality of fly ash which has been used for cement
and land fill.  Also, ammonia has been injected into the flue gas from the
No.2 oil-fired boiler between the air preheater and ESP in order to prevent
corrosion of ESP and to increase soot removal efficiency. Thus ammonia is
contained in the flue gas introduced into the No.2 FGD system, which has
also been operated without trouble.

     Chugoku Electric recently decided to install similar SCR and FGD
system for 5 relatively small existing coal-fired boilers.
                        5.   OTHER COMBINED SYSTEMS
 5.1  Takehara Plant,  EPDC

      EPDC has been constructing a full-scale demonstration plant of
 SCR combined with FGD at its Takehara Station for the No. 1 boiler
 (250 MW).  Since various types of coals including low-sulfur coal will
 be used,  a hot electrostatic precipitator is installed.  As shown in
 Figure 5, all of the flue gas from the boiler is passed through two
 parallel trains of a hot ESP, SCR reactor, air preheater and ID fan.
 One of the reactors is constructed by Babcock Hitachi Ltd. using a
 plate catalyst developed by Hitachi Ltd., while the other is constructed
 by Kawasaki Heavy Industries (KHI) using a tubular catalyst.  Over 80%


                                    103

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            Addition for demonstration test
                                                               J
B  Boiler,   APH  Air preheater,   ESP  Electrostatic precipitator

IDF  Induced fan,    HESP  Hot electrostatic precipitator

 Figure 5  Demonstration plant at Takehara, EPDC (250 MW)
   Conventional type
                                     Deposit
            Hot
Intermediate
Cold
                                                       Soot
                                                        blow
  Modified  type
   Soot
    blow
              Hot
    Combined Intermediate
             and cold
                              Soot
                               blow
Figure 6   Arrangement of air preheater elements
                           104

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of NOx will be removed maintaining leak NHj below 10 ppm.

     Since the air preheater treats an SOx-rich, dust-lean gas, ammonium
bisulfate may deposit in intermediate and low temperature zones
(Figure 6).  Pilot plant tests have shown that the deposit formed
between the two zones is difficult to remove by soot blowing.  For
the demonstration plant, a modified design of the air preheater
elements as shown in Figure 6 will be used to reduce the plugging
problem.

     The treated gas is sent to an existing FGD plant constructed by Bab-
cock Hitachi using the limestone-gypsum process (Table 3).   The leak
NH3 will be caught by the FGD system and contained in the wastewater.
EPDC has installed a wastewater treatment system using a conventional
activated sludge process to remove ammonia, because Takahara Station
faces the Seto Inland Sea which is sometimes plagued by the red tide
problem.

     The total additional system for the demonstration as shown in
Figure 5 cost 8 billion yen including control systems and a storage
and injection system of ammonia.  The new ID fans are estimated to
consume about 1,500 kW more than does the existing ID fans, which is
equivalent to 0.6% of the power generated by the boiler.

     EPDC will construct a full scale combined system for the new
No. 3 boiler  (700 MW), for which the low-dust system may also be applied.
5.2  Tomato-Atsuma Plant, Hokkaido Electric

     Hokkaido Electric Power Co. has constructed a new 350 MW coal-fired
boiler in a newly opened industrial region near Tomakomai, which has
started test operation in summer 1980 and is scheduled to be put in
commercial operation in October 1980 using a low-sulfur coal (S = 0.3%).
By an agreement with local governments, SOx emissions should be kept
below 180 Nm3/hr (about 140 ppm), NOx below 200 Nm3/hr (about 160 ppm),
and particulates below 200 kg/hr (about 160 mg/Nm3).

     For SOx abatement, half of the gas from the boiler is treated by
a wet limestone-gypsum process FGD plant constructed by Babcock Hitachi.
NOx is reduced below 200 ppm by combustion modification including staged
combustion, flue gas recirculation, and dual-register low-NOx burners.
In addition, one-fourth of the gas is treated by SCR for 80% NOx removal
to meet the agreement.

     Since a low-sulfur coal is used, a hot electrostatic precipitator
has been installed which reduces the dust content down to 45 mg/Nm3.
One-fourth of the gas passing through the hot ESP is treated by an SCR
reactor containing a plate catalyst developed by Hitachi Ltd.  An
economizer bypass system has been installed to maintain the gas
temperature above 300°C.

                                 105

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     Hokkaido Electric plans to install a 600 MW coal-fired boiler.
If the plan is authorized,  Hokkaido Electric plans to reevaluate
the design including the necessity of the bypass and the use of cold
vs. hot ESP.
5.3  Nakoso Plant, Joban Joint Electric Co.

     Tokyo Electric Power Co., jointly with Tohoku Electric Power Co.,
Joban Joint Electric Co., and MHI,  has carried out pilot plant tests
at Nakoso Station of Joban on combined systems of SCR (high-dust and
low-dust) and wet limestone-gypsum process FGD using 4,000 Nm^/hr
of flue gas from a coal-fired boiler.   In 1979, the high dust system
was operated for 5,000 hours while the low-dust system was operated
for 4,000 hours.  Further tests are in progress in 1980.

     Honeycomb catalysts are used for  both systems with downflow of
the gas.  With the high-dust system,  erosion of the catalyst by dust has
been prevented by placing on top of the honeycomb a dummy spacer which
has the same cross section as the honeycomb.  The air preheater has
been kept clean by applying soot blowing once a day; ammonium bisulfate
has not deposited appreciably because  of the cleaning effect of fly
ash.  With the low-dust system, the dust leaving the hot ESP is in a
small amount but consists of fine particles which are rather sticky
and tend  to deposit particularly at  the inlet of the honeycomb.
Moreover, the air  preheater requires  soot blowing 3 times a day to
prevent the deposit of ammonium bisulfate.

     The FGD system has been operated  without trouble.  A semiventuri
type spray scrubber developed by MHI  is used for the prescrubbing.  Tests
indicated that the dust contained in  the gas in concentrations of 100,
200, and 300 mg/Nnr* was reduced to about 20, 30, and 40 ppm, respectively,
by the prescrubber and to about 15, 20, and 30 ppm, respectively by
the S02 absorber.

     Joban has started to construct 2  new boilers with a capacity of
600 MW each, which will use low-sulfur oil with a small amount of coal
to start with.  Both boilers will have high-dust system SCR units with
a honeycomb catalyst.  The units for  one of the boilers will be
constructed by MHI and the units for  the other boiler by IHI.  FGD
plants may be constructed when larger  amounts of coal are used.
                                 106

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                       6.  OTHER MAJOR ACTIVITIES

                                                  3\
6.1  Pilot Plant Tests by Activated Carbon Process

     EPDC, jointly with Sumitomo Heavy Industries, has been operating
a pilot at Takehara with a capacity of treating 10,000 Nm3/hr of flue
gas from the No. 1 coal-fired boiler to remove over 90% of S02 and over
30% of NOx by activated carbon and ammonia.  A flowsheet of the pilot
plant is shown in Figure 7.  The flue gas containing 1,300 ppm of S02
and 320 ppm of NOx at about 150°C is injected with 225 ppm NH3 and is
introduced in a reactor with activated carbon in a moving bed.  Over
90% of S02 is adsorbed by the carbon to form sulfuric acid and ammonium
sulfate (reactions 1 and 2) while over 30% of NOx is converted to N2
(reaction 3).

     S02 + H20 + 1/2 02 •*• H2S04 	 (1)

     H2S04 + 2NH3       •*• (NH4)2S04 	 (2)

     4NO + 4NH3 + 02    + 4N2 + 6H20	 (3)


     The char loaded with the sulfur compounds is heated in a separate
moving bed to over 350°C by inert gas produced by incomplete combustion
of LPG gas.  Concentrated S02 gas is released by the heating (reactions
4 and 5), then is introduced into a coal-bed reactor and converted
to S by the Resox process developed by Foster Wheeler Co. (reaction 6).
The sulfur vapor is condensed to recover elemental sulfur.  The gas leaving
the condenser is incinerated and sent to the existing wet limestone-gypsum
process FGD plant.

     H2S04 + 1/2 C  -*• S02 + 1/2 C02 + H20  	 (4)

     (NH4)2S04 + 02 •*• S02 + N2 + 4H20 	 (5)

     S02 + C        ->• S + C02	 (6)


     About 1.6% of the carbon is consumed  in one cycle which takes
3 days.  The sulfur condenser had a plugging problem, which has been
solved by applying a technology used for the Glaus furnace.  The remaining
major problem is the low recovery of sulfur at 60 - 70%.  Efforts have
been made to improve the recovery.

     The low NOx removal efficiency is due to the low temperature.  Over
200°C with over 2 mole NH3 to 1 mol NOx may be needed to attain over
80% removal.  For commercial application,  it may be preferable to use
SCR for the boiler economizer outlet at 300 - 400°C and then apply
the carbon process for S02 removal only without using ammonia.  EPDC
                                  107

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No.l Boiler
                Electrostatic
Air Preheater   Precipitator
                                                              Pilot  plant
                                                                  Wet Desox

                                                                                    Stack
                                                     Coal
                                                        i
                                           Regenerator  J   Condenser
                                                                                         Tall gas
                                                                                          blower
         Ammonia injection
          unit
                                                        Inert  gas
                                                        generator
                                                                                Sulfur
                                                             Note:
                                                              	Gas

                                                              ____Activated
                                                                   carbon
                                                                                          Incinerator
               Figure 7  Pilot plant for FGH by activated carbon process for elemental sulfur recovery 3)

                              (Takehara f.3«ni-, F.PDC)

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is to install a prototype plant of the carbon process at its Matsushima
Station by 1982 to treat one-fourth of the gas from a new 500 MW
coal-fired boiler, while three-fourths of the gas will be treated by
the wet limestone-gypsum process.
6.2  New Combustion Technology

     About one-tenth of fuel used for the boiler is injected above the
combustion zone in the boiler to form a reducing atmosphere where NOx
formed by the combustion is reduced to N2-  Air is added above the
reducing zone for complete combustion.  The technology was originated
by MHI and has been further developed by Tokyo Electric Power Co.
jointly with MHI, Hitachi, and IHI for NOx abatement for boilers.
Tests with pilot plants with a capacity ranging from 5,000 to 8,000 kW
using various fuels have indicated that about 50% of NOx is removed.
By using the process in combination with conventional combustion
modification, NOx concentration has been reduced to 10 - 20 ppm with
gas, 40 - 60 ppm with oil, and 60 - 100 ppm with coal.  The boiler is
a little larger than a conventional boiler.  Tests on a larger scale
are planned.
                               REFERENCES
1.  Y. Nakabayashi, Plan, Design and Operating Experience of FGD For
    Coal Fired Boilers Owned by EPDC, Paper No. 41, EPA FGD Symposium,
    March 1979

2.  J. Ando, S02 Abatement for Stationary Sources in Japan, EPA-600/
    7-78-210, November 1978

3.  EPDC and Sumitomo Heavy Industries,.Simultaneous SOx-NOx Removal
    System for Coal-fired Boiler, October 1979
                                  189

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       Session 2: IMPACT OF RECENT LEGISLATION/REGULATIONS
                        Walter C. Barber, Chairman
                 Office of Air Quality Planning and Standards
                   U. S. Environmental Protection Agency
                   Research Triangle Park, North Carolina
            Panel:  Impact of Recent Legislation/Regulations
            Brief overviews of recent Legislation/Regulation,
            under the CAA, CWA, and RCRA, followed by
            questions from the audience.
            Members:  John W. Lum
                      Office of Water Planning and Standards
                      U.S. Environmental Protection Agency
                      Washington, D.C.

                      Penelope Hansen
                      Off ice of Solid Waste
                      U.S. Environmental Protection Agency
                      Washington, D.C.
            No papers or discussions are included for this session.
Preceding page blank

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           Sessions:-  FGD  RESEARCH AND DEVELOPMENT PLANS
                           Julian W. Jones, Chairman
                   Industrial Environmental Research Laboratory
                      U. S.  Environmental Protection Agency
                      Research Triangle Park, North Carolina
Preceding page blank
                                      113

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                   RECENT TRENDS IN UTILITY
                   FLUE GAS DESULFURIZATION
                             by

      M. P. Smith, M. T. Melia, and B. A. Laseke, Jr.
                 PEDCo Environmental, Inc.
                             and

                       Norman Kaplan
            U.S. Environmental Protection Agency
        Industrial Environmental Research Laboratory
            Emissions/Effluent Technology Branch
Preceding page blank
                             115

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                            ABSTRACT


     PEDCo Environmental,  Inc.,  under contract to the Industrial
Environmental Research  Laboratory-RTF  and the  Division of Sta-
tionary Source Enforcement of the  U.S.  Environmental Protection
Agency,  has  been  monitoring the  status  of  utility  flue  gas
desulfurization  (FGD)  technology  since  1974.   Information  for
this program is  obtained  by  visits to plants having operational
FGD systems  and  through periodic  contacts  with representatives
of utility companies,  FGD system and equipment suppliers, system
designers,  research  organizations,   and  regulatory  agencies.

     This paper  summarizes the  status  of utility FGD technology
as of the end of August 1980 and indicates recent trends in both
the design  and performance of the FGD  systems.   The discussion
of current status includes the number and capacity of operation-
al  and planned  FGD  systems, as well  as identification of  the
systems  according  to process  type,  emission control strategy,
S02  inlet  concentration  levels,   and  removal  efficiencies.
Process  design developments and trends are  summarized  for  the
major  components and  subsystems associated  with commercial  FGD
systems.  In discussing FGD system performance, composite graphs
are included presenting annual system availability data  (through
June 1980)  for low-,  medium-, and high-sulfur coal FGD instal-
lations.  A statistical analysis of  the data for the years 1978
and 1980  indicates  overall  trends in  FGD system dependability.
Finally,  capital and annual cost data  (both reported  and  ad-
justed)  are  included  for the operational FGD systems  and cost
model comparisons are made.

     The  current data  indicate that 203  FGD systems are either
operational,  under  construction,  or planned  (as of August 1980),
representing a total controlled capacity of about 97,000 MW.   Of
the 203,  73  systems are operational,  representing 27,155 MW of
controlled capacity.  The dependability analysis indicates that
the overall  median availability  for these  operational systems
has  increased  1.5%,  16.5%,   and  50.6%  for  low-,  medium-,  and
high-sulfur coal FGD installations,  respectively,  between  the
years 1978 and 1980.
                                116

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                              NOTES
1.    Company Names and Products.

     The mention  of  company names  or  products is  not to  be
     considered an endorsement or recommendation for  use by the
     U.S.  Environmental Protection Agency.

2.    Consistency of Information.

     The information  presented was  obtained  from a  variety  of
     sources  (sometimes by  telephone  conversation)  including
     system vendors,  users,  EPA trip reports and other technical
     reports.  As such, consistency  of  information  on a partic-
     ular system  and  between the several  systems discussed may
     be lacking.   The  information  presented is basically  that
     which  was voluntarily  submitted by  developers and  users
     with  some  interpretation  by  the  author.  The order  of
     presentation of  information or  the amount  of  information
     presented  for  any one  system   should  not be construed  to
     favor or disfavor that particular system.

3.    Units of Measure.

     EPA policy  is  to express all measurements in  Agency docu-
     ments  in metric  units.  When  implementing this  practice
     will result  in  undue cost or difficulty in clarity,  IERL-
     RTP provides  conversion factors for  the non-metric units.
     Generally, this paper uses British units of measure.

     The following equivalents can be used for conversion to the
     Metric system:

               British                  Metric

               5/9 (°F-32)              °C
               1 ft                     0.3048 m
               1 ft2                     0.0929 m2
               1 ft3                     0.0283 m3
               1 grain                  0.0648 gram
               1 Ib (avoir.)             0.4536 kg
               1 ton (long)             1.0160 m tons
               1 ton (short)             0.9072 m tons
               1 gal.                    3.7853 liters
               1 lb/106 Btu             429.6 ng/J
               1 Btu/kWh                1055.056 J/kWh


                                117

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                            SECTION 1

                          INTRODUCTION


     For  more  than  6  years  PEDCo  Environmental,  Inc.,  under
contract to the U.S.  Environmental  Protection Agency (EPA), has
monitored the development and growth of flue gas desulfurization
(FGD)  technology  for fossil  fuel-fired utility boilers  in the
United  States.   The program  provides  an objective  and current
perspective of  FGD technology  as  applied to  fossil fuel-fired
utility  boilers  and  facilitates,  through information  dissemi-
nation,  improvements  in the  design and performance of current
and future systems.

     The program  addresses  performance of  operational  FGD sys-
tems, process and design characteristics of both operational and
planned  systems,   projected  application  and  nature of  future
processes  and  systems,  and  costs  associated with both current
and planned  systems.   The program  also includes the monitoring
of particulate matter scrubbers  operating on coal-fired utility
boilers  in the United States  and FGD systems operating on coal-
fired utility boilers in Japan.

     Program emphasis is  on  the performance of the operational
systems.  Accurate portrayal of system performance requires data
concerning system/module  dependability, operating problems anci
solutions, operating and maintenance costs, and outlet emissions
and  removal  efficiency.   Data  on  outlet  emissions of  sulfur
dioxide  (SO2),  particulate matter,  and nitrogen oxides  (NO  ) and
on  removal  efficiency  of  S02  and  particulate  matter  are^ con-
sidered  information  needs  in  order  to  assess  actual  system
performance with respect to control requirements in  the recently
promulgated revised New Source  Performance Standards (NSPS) for
electric utility steam generating units.
     Utilities,  system  and  equipment  suppliers,  system design-
ers, research organizations, regulatory agencies,  and others all
volunteer  the   information  for  this  program.   This  voluntary
approach facilitates  timely dissemination of pertinent informa-
tion in  this  key  technological  area.   All  information that is
gathered is stored in a computerized data base known as the Flue
Gas Desulfurization Information  System (FGDIS).   This system is
discussed in more detail in Appendix A.
                                118

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     Information on  operational  systems  is verified  solely by
the utilities and reported essentially as received.  Any modifi-
cations or adjustments to  the  reported data are made solely for
purposes of a consistent format that will allow reliable compar-
isons and evaluations to be made.
                                 119

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                              SECTION 2

                         TECHNOLOGY OVERVIEW
CURRENT  STATUS

     Table 2-1  lists the  number  of domestic utility  FGD systems
according to  status  and  equivalent  electrical  capacities  as of
the end  of August  1980.
          TABLE 2-1.  NUMBER AND TOTAL CAPACITY OF FGD SYSTEMS,
                               AUGUST 1980
Status
Operational
Under construction
Planned:
Contract awarded
Letter of intent
Requesting/evaluating bids
Considering only FGD
TOTAL
No. of
units
73
39
29
7
15
40
203
Total
controlled
capacity, MW
27,155
17,855
13,769
5,590
8,424
24,200
96,993
Equivalent
scrubbed .
capacity, MW
24,765
16,854
12,919
5,590
8,424
23,980
92,532
  Total controlled capacity (TCC) represents the gross capacities (MW) of
  coal-fired units brought into compliance by FGD systems,  regardless of
  the percent of the flue gas treated.
  Equivalent scrubbed capacity (ESC)  represents the effective capacities of
  the FGD systems (in equivalent MW), based on the percent  of the flue gas
  treated.
GROWTH TRENDS

Power-Generating and  FGD Capacity

     As  indicated  in  Table  2-1,   73  coal-fired power-generating
units currently  equipped with operational  FGD systems represent
                                   120

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a total controlled capacity  of 27,155 MW..  This compares with a
December  1979  total  coal-fired  power-generating  capacity  of
approximately 235,000 MW.   Current projections indicate that the
latter will rise to approximately 370,000 MW by the end of 1990.
Based on the known utility commitments to FGD, the percentage of
coal-fired  capacity  controlled by  FGD  will  increase  from  its
current level of 11.5% to 26.5% by the end of 1990.

     Table 2-2 presents the projected distribution of power-gen-
erating  sources  (by energy  source)  in  the electric  utility
industry.   Table 2-3  presents  the  percentage  of current  and
projected   coal-fired   and  total  power-generating  capacities
controlled by FGD.

     Based  on  the  requirements  of  the  revised NSPS,  actual
FGD-controlled  capacity should  exceed the levels  indicated in
the preceding discussion.  Currently,  about 50 additional units,
representing  a  total capacity  of approximately  25,000 MW,  have
been  identified as  requiring S02  controls  in  the  decade  just
begun;  however,  identification  of  these  units  and information
regarding  their status  is not  ready for public release  as  a
result of the premature stage of  their planning, developments in
ongoing litigation, and the determination of applicable emission
control standards.

     Figure  2-1  shows  current  and  projected  FGD-controlled
capacity and total power-generating capacity of coal-fired units
through  1990.    This   figure  represents  the  committed  FGD-
controlled  capacity (those systems identified in Table 2-1), the
uncommitted FGD-controlled capacity (those units that cannot be
identified  at  the  present   time),   and  current  and  projected
coal-fired  power generating  capacities   (those  values cited in
Table 2-2 and the preceding discussion).

     Figure 2-2  shows estimated FGD-controlled capacities at the
indicated  month and year.   An estimated total  of 37,834 KW of
FGD-controlled  capacity  was  identified  in  November  1974.   By
August 1980, this figure had  risen to 96,993 MW  (see Table 2-1).
This  represents an overall  growth  rate  of  156% for the 6-year
period.   In  addition,  the  figures  reflect  a better  than 55%
increase in the  last 2 years.

     Other  notable changes that occurred  during the 1974 to 1980
growth period include:

     0    A 384% increase in the number  of operational systems.

     0    A 753% increase  in  operating capacity  (ESC).

     0    An  increase  in  the  average  capacity  of   the  FGD-
          equipped unit from  170  MW to 340 MW.
                                121

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            TABLE 2-2.   DISTRIBUTION OF  POWER-GENERATING SOURCES
                             BY  ENERGY SOURCE '

December 1979
December 1990
Percent of total
Coal
39
44
Nuclear
9
14
Oil
25
20
Hydro
13
11
Gas
13
10
Other
1
1
Total, GW
603
833
jj Adapted from U.S.  Department of Energy (1979)  and Rittenhouse (1978).1>2
  Figures reflect annual  losses of 0.4% of the year-end capacity attributed
  to retirement of older  units.
              TABLE 2-3.   FGD-CONTROLLED POWER-GENERATION CAPACITY
                               (percent of total)
Period
August 1980a
December 1990
Coal -fired
capacity
11.5b
26.5
Total capacity
4.5b
11.6
  Represents  FGD-committed  capacity as  of August 1980.
  Based on FGD capacity as  of  August 1980 and total  power-generating
  capacity as of December  1979.
                                       122

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450
400 -
350
300
250
200
150
100
 50
 I     I    I     I    I     I

COAL-FIRED CAPACITY

UNCOMMITTED FGD CAPACITY

COMMITTED FGD CAPACITY
  1975  76  77   78  79   80   81
                   82   83  84

                    YEAR
85  86   87
89   90
           Figure  2-1.  Projections of coal-fired generating
              capacity and FGD capacity from 1975 to 1990.
                                   123

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 o
 o
ro
 O
 (X
 
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Process  Type

     FGD systems may  be categorized in several  ways,  some gen-
eral and  others more  specific.   Some general  categorizations
used in  the survey  are:

     0     wet vs. dry process

     0     throwaway product vs.  salable product process

A more specific categorization  is  by process (e.g., lime, lime-
stone, magnesium oxide,  Wellman-Lord).

     Tables 2-4, 2-5,  and 2-6  summarize  the current  status of
FGD  capacities  associated with each  of  the foregoing  process
categories.  These  tables show that the vast majority of oper-
ating experience  to  date has  been  obtained with  wet calcium-
based,  throwaway-product  FGD systems.   Of the  68,044  MW of FGD
capacity committed to a specific process (see Table 2-6), 62,541
MW  (approximately 92%)  are  wet  calcium-based,  throwaway-product
systems.

     Table 2-4 shows  that all currently operating processes are
wet  systems.  With the recent  advent  of  spray  dryer collection
processes,  10 systems,  representing  an  ESC of 3,523  MW,  are
currently  committed  for  future  operation with a  dry  system.
Therefore, dry systems  represent  almost 12% of the FGD capacity
in  the  under  construction  and contract  awarded  status cate-
gories .

     Table 2-5  indicates that  approximately 6%  of the  current
operating  FGD-controiled capacity produces  a   salable  product
(elemental sulfur or  sulfuric acid).   This level of application
of  salable product processes is  expected to  remain relatively
unchanged  in the  near  future,  as reflected by the  7% and 9%
levels currently committed in the under construction and planned
status  categories.    In the  planned  category,  if  the   641 MW
scheduled  to produce  gypsum for sale are not considered  (gypsum
may have to be thrown away if a market is not available), the 9%
is reduced to 7%.

     Table  2-6  reflects  several  trends   in  the  industry  with
respect to chemical  process  selection.   Direct  lime  and lime-
stone systems  currently  account   for  approximately 89%  of the
chemical processes selected,  and a comparison of the two  shows  a
distinct  industry  preference  for  the latter,  which will get
stronger  in  the  near  future  as more  systems  are  placed in
service.   This  trend  is  evident in  that  53%  of  the lime/
limestone  capacity  in  operation,  59% of  the  lime/limestone
capacity  under  construction,  and  66%  of  the planned lime/
limestone capacity are limestone systems.*
* Includes alkaline fly ash limeyiimestone processes.

                                 125

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       TABLE 2-4.   COMMITTED FGD CAPACITY - WET VS.  DRY PROCESSES

Wet
Dry
TOTAL
FGD capacity (ESC), MW
Operational
24,767
0
24,767
Under
construction
15,194
1,660
16,854
Contract
awarded
11,056
1,863
12,919
Total
51,017
3,523
54,540
          TABLE 2-5.   DISTRIBUTION OF FGD SYSTEMS BY END-PRODUCT
                                 FGD capacity (ESC),  MW

Salable product
Throwaway product
TOTAL
Operational
1,600
23,167
24,767
Under construction
1,208
15,646
16,854
Planned
2,991a
29,678
32,669b
Total
5,799
68,491
74,290b
This total contains 641  MW of capacity which will  produce gypsum for sale
rather than sulfur or sulfuric acid.
This total is less than  that reflected in Table 2-1  because a number of
planned FGD systems have not yet been committed to a process.
                                     126

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             TABLE 2-6.   DISTRIBUTION OF FGD SYSTEMS BY PROCESS
Process
Limestone3
Limeb
Lime/spray drying
Lime/limestone
Sodium carbonate
Magnesium oxide
We 11 man Lord
Dual alkali
Aqueous carbonate/
spray drying0
Citrated
Total
FGD capacity (ESC), MW
Operational
11,172
9,869
0
20
925
0
1,540
1,181
0
60
24,767
Under
construction
8,816
4,940
1,120
0
330
574
534
0
540
0
16,854
Planned
16,164
6,035
1,907
475
250
750
0
842
0
Q
26,423e
Total
36,152
20,844
3,027
495
1,505
1,324
2,074
2,023
540
60
68,044
  Includes alkaline fly ash/1
,  configurations.
  Includes alkaline fly ash/1
  tions.
  Includes nonregenerable dry
d configurations.
  This system is operating at
  and is listed as a utility
,  a 25-MW interchange to the
  Because the processes of al
  in this status category are
imestone and limestone slurry process design

ime and lime slurry process design configura-

 collection and regenerable process design

 the St. Joseph Zinc Co., G. F- Wheaton Plant
FGD system because the plant is connected by
Duquesne Light Company.
1 planned systems are not known, the totals
 less than those in Table 2-1.-
                                      127

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Emission Control Strategy

     Emission  control  strategy  refers to  the  measures  used to
control particulate  matter and  S02  emissions from  power plants
firing  fossil   fuels.   At   FGD-equipped,   coal-fired   utility
boilers,   three   basic  combinations   of  primary   particulate
matter/S02  control  equipment are  used:   electrostatic  precipi-
tator  (ESP)/FGD,  fabric  filter (FF)/FGD,  and two-stage scrub-
bing.  Table  2-7  summarizes  emission control strategies for the
current and planned FGD-equipped units.
             TABLE 2-7.  SUMMARY OF EMISSION CONTROL SELECTION'

ESP/FGD
FF/FGD
Two- stage
scrubbing
Total
Operational
No.
46

27
73
MW
16,564

8,203
24,767
Under construction
No.
32
3
4
39
MW
13,890
990
1,974
16,854
Contract awarded
No.
22
7
0
29
MW
10,823
2,096
0
12,919
Total
No. .
100
10
31
141
MW
41,277
3,086
10,177
54,540
  Capacities represent ESC.
As  indicated  in Table  2-7,  several industry preferences  emerge
with  respect to  selection  of  a  control  strategy.   The  most
obvious  is the  strong  preference  to use  an  ESP  for primary
particulate matter control  upstream of the FGD  system.  Second,
a small but  increasing preference  for FF's is influenced  by the
advent  of the spray  dryer/dry collection  FGD technology.   The
suppliers  of most  of : the  dry processes  offered  commercially
recommend  a  FF  as the preferred  collection device.   All  the
FF/FGD combinations presented  in this table  are spray  dryer/dry
collection systems.   Third,  a preference  for  the  use of  two-
stage scrubbing system for SO2  and  particulate matter control is
diminishing.   The  units under construction  that will  use  two-
stage  scrubbing  are   either  retrofit  applications where  the
existing  particulate  matter control  devices (E'SP's)  need  lip-
grading  or  new  applications  where  the   alkalinity of  the
collected fly ash will be used  as a source of reagent.
                                 128

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APPLICATION CONSIDERATIONS

New/Retrofit Units

     Figure 2-3 shows  a  comparison of FGD-controlled capacities
with new and retrofit FGD systems.  As indicated in this figure,
many of the original FGD systems were retrofits (e.g., retrofits
accounted for 62% of the operating capacity in service in 1975).
As- of  August 1980, new  systems accounted  for  75% of the oper-
ating capacity.  This trend toward application of FGD systems on
new sources is a result of the NSPS promulgated, pursuant to the
Clean Air Act Amendments.  By 1990, FGD systems installed on new
boilers are expected to comprise 86% of the total.

Design SO9 Removal, Coal Sulfur Content, and Inlet S09 Level

     Tables  2-8  and 2-9  summarize the FGD systems  in service,
under  construction,  and planned  according  to  design values for
S02 . removal,   coal  sulfur  content,   and  inlet  S02  level.
Table  2-8 presents  a  breakdown  of  the  FGD  systems  that are
operational, under  construction,  and  planned (contract awarded)
according to level  of S02 removal efficiency versus coal sulfur
content.   Some general  statistics from the table are evident.
First,  more than  70% of the FGD capacity is  designed for S02
removal  efficiencies  of  80%  or greater  (almost  evenly  dis-
tributed  between  efficiencies   of 80  to  89%  and  the  90%  or
greater).   Second,  more than 85%  of  the FGD capacity installed
or planned  is  for  boilers  burning low-  and  high-sulfur coals,
with the  capacities almost equally distributed between the two.

     Table  2-9 presents a  breakdown  of FGD capacity by status
category  according to design inlet SO2  levels.  Establishing  4
lb/106  Btu  as  the  break- off level between low- and high-inlet
S02  leads  to  the  conclusion that  FGD systems  are used  to  a
greater  extent  on  low-level  S02  inlets  than  on high-level
inlets.  Since 56% of present operational capacity is applied to
low-inlet SO2  levels,  as are 62%  of the systems under construc-
tion,  and 64% of  the planned systems,  it appears that more of
the  future  coal  fired utility units are expected  to use low- or
medium-sulfur  coal with FGD than high-sulfur coal  and FGD.  This
may  be because  there is  more  coal-fired  utility growth where
low- or medium-sulfur coal exists.
     Note that the preferences  and trends cited  in Tables 2-8
and  2-9 virtually exclude any  impact  that may be brought  about
by the  revised NSPS of June 1979.  This discussion  is therefore
limited  to  technological preferences  and trends that developed
largely  in  response  the Federal,  state,   and  local regulatory
standards under the original NSPS  of December 1971.
                                 129

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CO
 o
 o
 <
 a.
 co
 CD
 a:
 UJ
 a.
 o
      1975  76   77  78   79  80   81   82  83   84   85   86   87   88   89   SO

                                         YEAR
    Figure 2-3.  Committed FGD operating  capacity for new and retrofit

                       installations through  1990.
                                      130

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        TABLE 2-8.  DESIGN S02 REMOVAL EFFICIENCIES OF  FGD  SYSTEMS
                    WITH RESPECT TO COAL SULFUR CONTENT
Design
removal
efficiency
< 70
Total
70-79
Total
80-89
Total
> 90
Total
TOTAL
Coal sulfur
content3
Low
Medium
Hi ah

Low
Medi urn
High

Low
Medium
Hiqh

Low
Medium
Hiah

Low
Medium
High
Operational
No.
7
7
0
14
6
1
4
11
13
2
12
27
6
3
12
21
32
13
28
MWb
3,066
1,306
0
4,372
2,359
800
1.180
4,339
3,938
918
4,181
9,037
2,044
749
4,225
7,018
11,407
3,773
9,586
Under
construction
No.
2
1
0
3
3
1
1
5
2
3
8
13
6
3
9
18
13
8
18
MWb
767
280
0
1,047
1,262
382
500
2,144
1,017
1,080
3,557
5,654
3,200
544
4,265
8,009
6,246
2,286
8,322
Contract awarded
No.
0
0
0
0
7
0
0
7
6
2
4
12
2
2
6
10
15
4
10
MWb
0
0
0
0
3,273
0
0
3,273
3,303
1,000
1,955
6,258
800
530
2,058
3,388
7,376
1,530
4,013
Total
No.
9
8
0
17
16
2
5
23
21
7
24
52
14
8
27
49
60
25
56
MWb
3,832
1,586
0
5,419
6,894
1,182
1,680
9,756
8,253
2,8io
9,693
20,949
6,044
1,823
10,548
18,415
25,029
7,58r
21,921
  Low-sulfur content  is  less  than  1%;  medium-sulfur content is  1  to  2.5%
.sulfur;  high-sulfur content is greater  than  2,5%.
  Capacities represent ESC.


                   TABLE 2-9.   FGD SYSTEM S02  INLET LEVELS
FGD system S02
inlet
(Tb/106 Btu)
< 1.9
2.0 - 3.9
4.0 - 5.9
> 6.0
TOTAL
Operational
No.
26
18
8
21
73
MWa
8,636
5,235
4,260
6,635
24,766
Under
construction
No.
10
10
4
15
39
MWa
5,039
2,933
1,204
7,678
16,854
Contract awarded
No.
12
5
10
2
29
MWa
5,856
2,520
3,743
800
12,919
Tota^
No.
48
33
22
38
141
MWa
19,53''
10,688
9,207
15,113
54,539
  Capacities  represent  ESC<
                                       131

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                            SECTION 3

                   PROCESS DESIGN DEVELOPMENTS


     This  section  addresses  preferences  and  trends  in  the
process design development of  commercial FGD systems.


CHEMICAL ADDITIVES

     Chemical  additives are  used  to  improve  the  chemistry of
lime- and  limestone-based  FGD systems.   For example, magnesium-
promoted processes have been used to reduce scaling, to increase
sulfur  dioxide  removal,   and to  improve reagent  utilization.

     Table 3-1 lists the number  and generating capacity of units
that now  have or will  have  FGD  systems  with magnesium-promoted
processes.
       TABLE 3-1.  NUMBER AND CAPACITY OF UNITS USING MAGNESIUM-PROMOTED
                             FGD PROCESSES
Process
Lime
Limestone
Lime/alkaline fly ash
Total
Operational
No.
7
0
0
7
MWa
4,433
0
0
4,433
Under construction
No.
2
1
2
5
MWa
860
670
1,400
2,930
Contract awarded
No.
0
1
0
1
MWa
0
650
0
650
  Equivalent scrubbed capacity.
     The  introduction  of magnesium into  lime- -and limestone-
based FGD processes  has been of  great interest over the last 10
years, but  most full-scale  magnesium-promoted  systems actually
began operations in  the mid  to late  1970's.  Table  3-1 shows
that  the  trend in the  use  of magnesium promotion is declining.
                                 132

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SYSTEM ENERGY CONSUMPTION

     Table 3-2  shows  the  range  and  average of  energy require-
ments of  lime  and limestone processes  as a percentage of gross
generating capacity  for new and  retrofit systems.   As shown in
the table, there  is no  significant  difference between  new and
retrofit systems.


       TABLE  3-2.  ENERGY  CONSUMPTION FOR OPERATIONAL  WET LIME AND
                     LIMESTONE SCRUBBING SYSTEMS3

Process
Lime
Limestone
Newb
Range
1.6 - 6.0
1.1 - 5.5
Average
3.8
3.2
Retrofit13
Range
1.5 - 3.5
3.4 - 5.6
Average
2.6
4.6
Overall
Average
3.1
3.4
  Excluding flue gas reheat.
  Electrical energy consumption of the FGD  installation as a percentage of
  gross.
FANS

     Table 3-3  shows the  trends in  fan preference  used on FGD
systems.   Although most of these  fans are centrifugal, utilities
are  considering  more innovative  designs.   Because early  FGD
systems were considered separate  from the rest  of the generating
plant,  separate  booster  fans  provided  draft for  the scrubbing
systems.   Newer  power plants  have fans  sized  to  provide draft
for  the  entire boiler/scrubber installation as a  unit.  Where
ESP's or  baghouses provide  particulate matter  removal  prior ro
the  scrubbing  system, forced-draft  fans (with  respect  to  the
scrubber) are used extensively.  These  fans  operate on dry flue
gas.  Most  induced-draft  (ID)  fans  operate  on dry  flue gas as
well because they are often  installed downstream from reheaters.
Carbon steel  is now and will  continue  to  be  the  primary con-
struction material for fans.


ABSORBERS

     Table 3-4  is  a breakdown  of the  number  and  capacity of
units equipped  with  FGD  systems according  to  generic  absorber
type and  status.   Combination absorbers  include spray/packed and
tray/packed absorbers as  well  as concentric  venturi/spray tower
absorbers.  Impingement  towers  are  fixed-baffle  or fixed-vane
                                133

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       TABLE  3-3.   NUMBER  AND  CAPACITY  OF  UNITS  BY FAN SPECIFICATION
                          AND  INITIAL STARTUP  YEAR
Fan specification
Design
Centrifugal
Axial
NRe
Function
Unit
Booster
NRe
Application
IDC
FDe
NRe
Service
Wet
Dry
NR
Materials
Alloy
Carbon steel
Rubber- lined
carbon steel
NR
a
Year of actual or projected FGD system initial startup
1971-1974
No.

8
0
3

3
5
3

7
2
2

1
8
2

1
8
0
2
MWa

2,198
0
145

191
1,199
945

2,073
250
20

408
1,915
20

408
1,915
0
20
1975-1978
No.

31
1
1

21
11
1

10
23
0

3
30
0

3
28
2
0
MWa

12,529
185
200

9,623
2,849
442

4,041
8,873
0

2,344
10,570
0

2,344
9,850
720
0
1979-1982
No.

34
4
37

13
22
40

11
40
24

6
49
20

3
47
0
25
MWa

12,880
1,313
14,315

5,417
7,482
15,609

3,833
16,411
8,264

1,820
19,433
7,255

1,141
18,443
0
8,924
Equivalent scrubbed capacity.
With respect to the FGD system
Induced draft.
Forced draft.
Not reported.
                                     134

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absorbers,   such  as  the  disc  contactor   design.    Fixed-  or
static-bed,  mobile-bed,  and  rod-deck absorbers  are  considered
packed towers.   Systems in which  flue gas  is contacted  with a
slurry or  solution  such  that  the   flue  gas  is  adiabatically
humidified and the  slurry or solution is evaporated to apparent
dryness  are  defined  as  spray  dryers.    Both  horizontal  and
vertical  spray  absorber  modules,  which  use  radial,  central,
cocurrent,  countercurrent, or  crosscurrent spray  arrangements,
are considered spray towers.  Impingement,  sieve,  and valve tray
absorbers  are  considered  tray towers.   Fixed-  and  variable-
throat venturi scrubbers as well as  other  absorber designs that
operate  on  a  venturi  principle  are  grouped   under  venturi
absorbers.
    TABLE 3-4.  NUMBER, CAPACITY,  AND STATUS OF UNITS EQUIPPED WITH FGD
                        SYSTEMS BY ABSORBER TYPE
Absorber type
Combination absorbers
Impingement tower
Packed tower
Spray dryer
Spray tower
Tray tower
Venturi absorber
Operational
No.
10
1
19
0
20
15
8
MWb
3269
265
6265
0
7181
4396
3391
Under construction
No.
6
0
8
5
16
3
1
MWb
2871
0
3211
1660
7075
1802
235
Contract awarded
No.
3
2
2
6
15
1
0
MWb
1391
842
750
1863
8008
65
0
a These totals include S02 absorbers. Parti cul ate matter scrubbers are
b excluded.
Equivalent scrubbed capacity.
     Table  3-4 indicates  that spray towers have  retained their
popularity  and that spray dryers will become more  prominent in
the  1980fs.   Except for Venturis, which  are on the decline, and
these two prominent designs, the  other  absorbers  show no marked
change in commercial acceptability.


MIST ELIMINATORS

     Utilities  and system  designers   apparently  prefer  mist
eliminators  of the chevron design,  particularly when  they are
preceded by  a bulk  separator.   The primary material of construc-
tion  is plastic,   although some  mist  eliminators  are  made of
                                 135

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alloys.   None of those  in  the contract awarded  status and only
one unit  now  under construction will be constructed of materials
other than plastic.
     Most mist  eliminators  are horizontal,  that  is  they are
installed perpendicular to  the vertically rising gas stream of
conventional  vertical  absorbers.  Vertical mist  eliminators are
used in  horizontal  absorber modules  and some vertical absorbers
that have a  90-degree  turn of  the  duct  (and  thus  a horizontal
duct section before entry  into the  stack).  The  advantage of a
vertical  mist eliminator is that the liquid collected is removed
perpendicular to the gas flow rather than opposite  to it, thus
improving the  liquid  removal  efficiency.   These patterns are
somewhat  evident in Table 3-5.
               TABLE 3-5.  NUMBER AND CAPACITY OF FGD-EQUIPPED
     UNITS BY MIST ELIMINATOR TYPE, CONFIGURATION, AND INITIAL STARTUP YEAR

Type
Chevron
Mesh-pad
Radial -vane
Configuration
Horizontal
Vertical
Year of actual or projected FGD system initial startup
1971 - 1974
No.

10
1
2

11
0
MWa

2,202
no
250

2,323
0
1975 - 1978
No.

34
1
1

28
6
MWa

12,106
360
125

10,355
1,418
1979 - 1982
No.

38
0
1

17
5
MWa

14,929
0
475

6,663
1,793
  Equivalent scrubbed capacity.
REHEATERS

     Four reheat  strategies are currently  in use or planned for
domestic  utility  FGD  systems:    flue   gas   bypass,  direct-
combustion,   hot-air-injection,  and  in-line reheat.   In direct-
combustion systems, fuel oil or gas  is  burned and hot combustion
products are mixed with the  wet  scrubbed gas  before it enters
the  stack.   Hot-air-injection  systems heat  ambient  air  on the
shell side of a steam tube  heat exchanger and inject it into the
flue gas  stream.   In-line reheaters  heat  the  flue  gas  as  it
passes through  the duct and  contacts the  reheater tubes.  Both
of the latter two systems use steam  tubes with circulating steam
                                 136

-------
or pressuri2ed hot water for heat transfer.   In  some  instances  a
unit will combine reheat systems.   For  example, where the  per-
cent of gas scrubbed  can be made to  vary with coal  sulfur  con-
tent/  the flue gas is reheated by bypassing the  particle-cleaned
gad around  the scrubbing system  to  the  scrubber exit ductwork
until the  amount of  allowable bypassed  gas  becomes  inadequate
for the  required degree of reheat  (when  the percent sulfur  is
high), at  which  point a backup  hot-air-injection  reheater  is
activated.

     Another variation of the basic reheater is the  waste-heat
recovery reheater.   A waste-heat  recovery reheater on a  system
currently  under  construction  is  an  in-line  reheater  that
includes two  heat transfer areas.   In the first transfer area,
upstream of the scrubber,  heat  is  absorbed  from the flue  gas;
water  circulating through  heat  exchanger tubes  transfers  the
heat  to  a  second transfer  area  downstream  from the scrubber.

     Table 3-6  is a breakdown of the reheat processes reported
by  number  and  capacity of  units where  these  systems  are  in-
stalled or planned.
          TABLE 3-6.  NUMBER, CAPACITY, AND STATUS OF UNITS USING
                      FLUE GAS REHEAT STRATEGIES
Reheat type
Bypass
Bypass/hot air injection
Di rect-combusti on
Hot-ai r- i n jecti on
In-line
Waste- heat recovery
Operational
No.
19
1
10
21
14
0
MWa
7,149
447
2,589
6,738
5,441
0
Under construction
No.
10
1
1
6
3
2 J
MWa
4,661
447
240
2,570
1,375
1,408
Contract awarded
No.
2
0
0
3
3
0
MWa
1,320
0
0
1,475
286
0
  Equivalent scrubbed capacity.


     Five units  (1687 MW)  that are  operational,, one unit  (110
MW)  that is  under construction,  and five  units (1416 MW)  for
which  contracts   have been  awarded  do  not include  reheaters.


STACK FLUES

     Table 3-7 is a breakdown of units  according to  materials of
construction of the stacks, status, and whether or not they have
reheat.  The flues of most stacks are and continue to be made of
                                137

-------
                  TABLE 3-7.  NUMBER, CAPACITY, AND STATUS OF UNITS EQUIPPED WITH FGD SYSTEMS
                              ACCORDING TO FLUE/LINER TYPE AND REHEAT APPLICATION


Flue/liner
Alloy
ARBMb
Carbon steel
C.S. /inorganic lining
C.S.c/organic lining
Fiberglass
HCBCd
Operational
With reheat
No.
0
19
5
2
7
2
10
MW°
0
6103
2976
1834
2369
455
2370
Without reheat
No.
1
6
0
1
2
0
0
MW
917
2015
0
98
514
0
0
Under construction
With reheat
No.
0
11
0
0
0
3
1
MWa
0
5472
0
0
0
1220
242
Without rehe.at
No.
0
4
0
0
0
0
0
MWa
0
1455
0
0
0
0
0
Contract awarded
With reheat
No.
0
4
0
0
0
2
0
MWa
0
1426
0
0
0
1000
0
Without reheat
No.
0
3
0
0
0
0
0
MW
0
1687
0
0
0
0
0
.  Equivalent scrubbed capacity.
  Acid resistant brick and mortar.
j Carbon steel.
  Hydraulic-cement-bonded concrete.

-------
acid-resistant brick  and  mortar  (ARBM).   Information regarding
materials of construction in  the  units under construction or on
which contracts have  been awarded  is  lacking partially because
utilities often do  not finalize stack design  until  late in the
construction stage.
SLUDGE DISPOSAL

     Table 3-8 is a breakdown of units equipped with FGD accord-
ing to sludge  treatment,  transportation,  disposal method, site,
and operational  status.   As in the  case  of stacks,  information
on units  under construction and on  which contracts  are awarded
is incomplete  because final  disposal strategies  are  often not
finalized until  plant construction  is nearly  complete.   Also,
when a separate  contract  is arranged for sludge disposal, it is
often-not awarded until after initial plant construction.

     Most disposal  sites  are  and will  continue  to be  on the
plant site.   One trend is to increase sludge solids content by
fly ash addition and/or using vacuum filters so the material can
be landfilled.   Another trend  is  to provide some  sort of sludge
treatment before final disposal;  primary  methods are  fly ash
stabilization, forced  oxidation,  and proprietary fixation.  As
more  systems  produce  sludge  with higher  solids  content,  waste
transport  by  truck  and/or  conveyor  belt  will  become  more
prominent.
                                 139

-------
       TABLE 3-8.  NUMBER, CAPACITY, AND STATUS OF UNITS EQUIPPED WITH  FGD
         SYSTEMS ACCORDING TO SLUDGE DISPOSAL SPECIFICATIONS AND STATUS
Disposal specification
Sludge treatment type
Bottom ash addition
Fly ash/lime stabili-
zation
Fly ash addition0
Fly ash mixing
Forced oxidation
Proprietary fixation
Sludge transportation
Conveyor
Pipeline
Rail
Truck
Sludge disposal method
Landf i 1 1
Lined pond
Mine fill
Unlined pond
Disposal site
Onsite
Off site
Operational
No.

1

5
9
3
4
11

4
29
3
12

21
30
2
14

55
14
MWa

490

956
3,494
1,785
2,025
5,615

1,070
10,666
1,785
3,526

9,011
9,408
632
3,971

15,915
4,899
Under construction
No.

0

0
0
3
6
6

2
1
1
6

16
9
3
0

17
4
MWa

0

0
0
1,219
3,430
2,686

1,140
280
500
2,733

7,858
3,943
1,421
0

8,002
1,397
Contract awarded
No.

0

1
0
2
1
2

0
0
0
5

10
1
0
0

2
2
MWa

0

65
0
1,000
166
1,370

0
0
0
2,146

3,824
50
0
0

1,067
120
b Equivalent scrubbed capacity.
c FGD wastes and bottom ash are  disposed of together.
d FGD wastes and fly ash are disposed of together.
  FGD wastes and fly ash are mixed before final  disposal.
                                      140

-------
                            SECTION 4

                       PERFORMANCE TRENDS
OPERATING EXPERIENCE

     In the past  5  years,  FGD has become  the  most commercially
(developed means  of  control  of  S02  emissions  from  coal-fired
boilers,  and operating  experience has  increased significantly.
At the end of  1975,  20  units were either on line (or had been),
and approximately 198,000  hours  of on-line  experience had been
accumulated.   By  August 1980, 85 FGD systems  had been operated
on utility boilers,  and more than 460,000 hours of operation had
been logged.   This  represents a  425% increase  in the number of
FGD systems operated and a 230%  increase in total hours logged.

     The operational  hours  above  reflect the  number  of  hours
reported by the utilities.   Because hours of operation often are
not available for such periods as initial system startup or per-
formance  testing,  the  actual number  of  operational  hours  is
greater  than  reported,  as  is   the  corresponding  percentage
increase.
DEPENDABILITY

     For characterization  of system performance,  four dependa-
bility parameters have been  developed:   availability, operabil-
ity,  reliability,   and  utilization.   Table  4-1  defines  these
parameters.

     The FGD survey program  includes monitoring the performance
of  the  operating   FGD  systems  and  logging monthly operating-
parameters (e.g., boiler and FGD system operating hours, forced
outage  times,  scheduled  outage  times).    If the  data  permit,
monthly  dependability parameters  are  calculated  for both the
entire FGD system and its respective modules  (where applicable).
When modular  operating parameters  are  known, total  FGD system
dependability  parameters  are  derived  by   averaging  all  the
modular  figures,  except  in  those  cases  where  the  FGD system
design  includes  spare capacity.   In these  instances,  a  spare
capacity  factor  is  included  in the calculation  of  the  total
system  parameter,  which  ensures  that  the  overall  FGD system
dependability  is  not  penalized  as   a  result  of  equipment
redundancy.
                                141

-------
                   TABLE 4-1.   PARAMETERS OF DEPENDABILITY
Availability index



Operability index


Reliability index


Utilization index
Hours the FGD system is available for operation
(whether operated or not) divided by the hours in
the period.

Hours the FGD system was operated divided by the
boiler operating hours in the period.

Hours the FGD system was operated divided by the
hours it was called upon to operate.

Hours the FGD system operated divided by the
total hours  in the period.
                                      142

-------
     Figures  4-1  and 4-2  reflect the  availability history  of
four FGD installations  on boilers firing  low-  or medium-sulfur
(<2.5%)  coal, and  Figures 4-3 and 4-4 show  the availability of
four FGD  installations  on boilers  firing  high-sulfur  (>2.5%)
coal.  These units  represent systems for  which sufficient data
jare  available  for  analysis.    In each  case,   the data  points
represent 12-month rolling averages  of  the monthly total system
availabilities.    The   rolling   averages   are   calculated   by
averaging the  availability  data  for  the  first  12  months  of
operation,  dropping  the first data  point,  and adding  the 13th
for a second average, and so on.

     Figures 4-5, 4-6,  and 4-7  are composites of the availabil-
ities  of individual FGD systems.   They  show  average  annual
availabilities (through June 1980)  for operating units firing
low-sulfur  (<1%)  coal,   medium-sulfur  (1-3%)  coal,  and  high-
sulfur  (>3%)  coal,  respectively.*   Some  newly operational sys-
tems were not included (even though data were available) because
they had been  in operation  for  less  than  1  year and yearly
availability averages were not available.

     Figure 4-8  provides statistical analyses  of the  data con-
tained in the three composite graphs for 1978 and 1980.   In each
case, the availability  points for these two years were plotted,
and  the median  of each  array  was  determined.   Note  that  the
median  FGD  system  availability  for those  systems applied to
units firing high-sulfur (>3%)  coal .has shown a better than 50%
increase in  the  2-year  period,  and is  approaching that of the
low- to medium-sulfur coal units.  This indicates  a rising trend
in the overall dependability of FGD systems for high-sulfur coal
application.  The  median availability for  units firing medium-
sulfur  (1-3%)  coal increased 16.5%  and,  for units firing low-
sulfur  coal,  1.5%.   The  lower  percent  change  for these  two
categories is  attributable  to  their higher median availability
in  1978  and  attests  to  the   stable   and  reliable  operating
histories experienced by FGD systems on  these  low- and medium-
sulfur coal units.
S02 REMOVAL EFFICIENCY

     Table 4-2 presents  S02  removal efficiency performance test
results  and  total system  design removal  efficiency values  for
some of the operational FGD systems.  Table 4-3 presents contin-
uous monitoring data  for some of these systems.  All but two of
the  systems  represented  in  these  tables are  commercial  lime/
*
  These  categories were used  to provide  a  more even graphical
  distribution; however, they differ slightly from those used in
  previous sections.
                                143

-------
3
i
  40
         I I I I  I I I1
                                      I I I  I I
     I I I  I I I I  1 I I 1  I I I I  I 1 I  I I I I  I I 1 1  I I I  I I I I  I I I  I I I I  I I I  I I I  I I I I  I I I  I I 1 I  I

    JFHAHJJASOKOJfHAMJJASONDJfMAHJJAiONDJFMAHJJASONDJFHANJJASOND

          1476              1977             1976             1979              1980

                                        ItAK
                                   Col strip 1
         100
              I I I  I I I I  I I I I  I I I I  I I I  I I I I  I I 1  I I 1 I  l I 1  I I l I  l i !  l I l  I l l

           JfKAHJJASOHOJfM»HJJASOIIOJIHAKJJA50NOJFHAMJJASOI(D

                 •»»              1978              1979             1960
                                   Colstrip  2

      Figure 4-1.   Availability histories  for FGD  installations  at the
                Colstrip Station of Montana Power (£2.5% S coal).
                                        144

-------
  100
  M>
E
§
I
  20
     l i  i i l i  i i i  i i I l  l l i l  i i i i  i t I  t i i i  i i i t  l l t I  i 1 t  l | I I  1 i I

    JfHANJJAiONOJFHAMJJAiUNOJINAHJJAiONOJFMAHJJASONl)

          1977             197*              1979              19UO

                                 YUR
                            Sherburne 1
          100
        S M
          40
             I I  I l I I  1 i l  l l I I  I I I I  1 I l  I I I I  I I I I  I I I  I 1 I

            JfMAMJJASOkOJFMAMJJAiONUJFMANJJASOND

                  1*7*             1979              I960

                                 TtAt
                             Sherburne 2

            Figure 4-2.  Availability histories for FGD
                  installations at the Sherburne Station
              of Northern States Power (<2.5% S coal).
                                 145

-------
  100
  BO
      	.. i  i !..i  i .... i I .. . . . i  i i i i  i i i i i  i i i i  i i i I   Bruce Mansfield 1
    JFHAHJJASOIIOJfHAHJJASONDjrMAMJJASONOJFMANJJASOIIO
          U77             1978             1979              I960
       I  1 I I I I I I I I  I I I I I  I
                               I I I I I
     l l  l . l l l  l l t l I  l i l i  | 'l \ . i  i | I i  i l l i  l l 1 l  I

    JfHAHJJASONOaFKAHJJASONDJFMAKJJASOND
          1978              1979             1980
                                             Bruce Mansfield 2
  100
p
i
i i i
   JFMAHJJASONOJfHAMJJASOHOJFMAHJJASONO
         '»'•             1979             mo
                                                  Widows Creek 8
        Figure 4-3.  Availability histories for FGD  installations
          at the Bruce Mansfield Station of Pennsylvania  Power
  and Widows Creek Station of  Tennessee Valley Authority (>2.5% S  coal)

                                     146

-------
too
80
60
20
                                                                      I  I I
                                                                                   i i
                                                                                            i I i i i i i
  •JFHAKJJASON
        1974
DJfNAMJJASOHLJF
       1975
MAMJJASONOJf
    1976
MAHJJASONDjr
    1977
MANJJASONDJ
    1978
                                                                               r H A
i .1 J • s n
 1S79
                                                                                            pjr HAUJJASOIIP
         Figure 4-4.
       Availability history  for the FGD  Installation at  the LaCygne  Station
           of Kansas City Power and Light (>2.S% S coal).

-------
                                                                    -LAWRENCE 5
      100
            REID GARDNER 1
/
       80
  S   60
  en
  «=t
       40
       20
                                             SAN JUAN 1
                                             SAN JUAN 2
                                             APACHE 2
             COLSTRIP 1
        1974
                                                                                       COAL CHj|
1975
                                                                                       JIM I
                          'INITIAL  SYSTEM AVAILABILITY AVERAGE.
                           1             I             1         '
1976
1977


YEAR
1978
1979
1980
                  Figure 4-5.  Annual  average availability histories for
                          low sulfur  (<1%) coal FGD  installations.
                                              148

-------
   100 -
    80
5    60
CO
     40
     20
          ®=INITIAL SYSTEM AVAILABILITY AVERAGE.
          	I	I	I
                                      R.D. MORROW, SR. 2
                                     R.D. MORROW. SR. 1
      1974
1975
1976
1977

YEAR
1978
1979
1980
              Figure 4-6.   Annual average availability  histories  for
                  medium sulfur (1-3%) coal FGD installations.
                                        149

-------
d    60
CO
<:
     40 -
     20 -
                          LA CYGNE 1
                       GREEN RIVER 1-3
                                                                        A.B. BROWN 1
              INITIAL SYSTEM AVAILABILITY  AVERAGE.

                    1	_J	     I
1974        1975        1976
                                                       1977


                                                       YEAR
1978         1979
                   Figure 4-7.  Annual  average availability histories  for
                          high  sulfur  (>3%)  coal  FGD installations.
                                              150

-------
100
80
•*
i-
1
M 40
cn
*-•
20
	 1 	 r- 	 1 	
-
•
— «•

-
-
1978 1979 1980
100
80
M
I 60
|
40
20
i l i
* !
t •
•
* •

-
-
1978 1979 1980
100
80
•*
| 60
1
40
20
i i l
I

_
: i
-
i i i
1978 1979 1980
YEAR YEAR YEAR
    MEDIAN = 93.45       MEDIAN = 94.85
              * CHANGE IN
             MEDIAN =1.5%
    MEDIAN * 77.65       MEDIAN ' 90.50
              X CHANGE IN
             MEDIAN = 16.51
MEDIAN = 53.50       MEDIAN = 79.05
          S CHANGE IN
         MEDIAN = 50.61
Low  sulfur coal installations.
Medium sulfur  coal installations.         High sulfur coal  installations.
       Figure  4-8.  Statistical  analyses of the annual  availability data  for the  years  1978 and  1980.

-------
                           TABLE 4-2.  S02 REMOVAL EFFICIENCIES; PERFORMANCE  TEST  DATA
tn
Utility name/
unit name
Arizona Public Service
Choi la 1






Duquesne Light
ohillips 1-6


Kansas City Power & Light
LaCygne 1







Kansas Power & Light
Lawrence 4


Kentucky Utilities
Green River 1-3


Louisville Gas & Electric
Can Run 4



Can Run 5


Cane Run 6



Montana Power
Colstrip 1



Colstrip 2



it i nuprl^
Unit rating,
HW (gross)

119







408



874








125



64



188



200


299




360



360




Process
type

Limestone







Lime



Limestone








Limestone



Lime



lime



Limestone


Dual alkali




Lime/alkalins
f lyash


Lime/a 1 kal in*
flyash



Fuel sulfur
content, %

0.5







1.5



5.4








0.6



4.0



3.8



3.8


4.8




0.8



0.8




Design removal
efficiency, %

92a







83b



80








73



80



85



85


95




60



60




Date

10/73


10/73




1975



3/75


5/75


8/77


10/77



10/78



3/77

8/77

7/79


7/80




2/76
1/77
5/77
6/77
10/76
11/76
l?/76
3/77
r>/77
Performance
test results, %

92


58.5




86-93



77


80


77


96-98



83



95

86-89

88


94




75
81
88
81
68
83
83
86
83
Remarks

Test results are based
on testing of Module
A only
Test results are based
on the average of
tests from October 2,
to October 21 , 1973

Tests results are from
two-stage scrubbing
train

Test results were
taken from a 4-hour
full load test
Results are based on
an 8-hour maximum
continuous load test
Summary of a 4-hour
full load test

Summary of overall
results from accept-
ance tests

Results are the
average of six test
runs

Results of a 7- to
10-day test period
Performance test re-
sults
The result is an aver-
age of three emission
tests
The result is from
compliance test per-
formed over an 11-
day period

Tests were EPA Method
6 procedures


Tests were EPA Method
6 procedures




-------
TABLE  4-2  (continued)
Utility name/
unit name
Northern Indiana Public Service
O.H. Mitchell 11







South Mississippi Elect. Power
R.D. Morrow. SR. 1





Springfield City Utilities
Southwest 1

Texas Utilities
Martin Lake I




Unit rating,
MW (gross)

115








200






194


793




Process
type

Wellman Lord








Limestone






Limestone


Limp stone




Fuel sulfur
content, %

3.5








1.3






3.5


0.9




Design removal
efficiency, X

90








85C






80


95d




Date

9/77








3/80


4/80



9/77


6/77


8/78

Performance
test results, X

91








92


90



92


98-99


98-99

Remarks

Tests commenced on
Aug. 29, 1977, and
were completed on
Sept. 14. 1977. test
period included 12
days at 92 MW flue
gas equivalent and
3-1/2 days at 1 10 MW
flue gas equivalent
Results of five EPA
Method 6 tests across
the absorber
Results of seven EPA
Method 6 tests across
the absorber

Average result of co»-
pliance test runs

Preliminary acceptance
test results at 750
MW
Acceptance test
results
  b Module  A removal efficiency; overall unit design removal  efficiency is 59%.
    Design  removal efficiency of the two-stage scrubbing trains.
   . Absorber design removal  efficiency; overall  removal efficiency  is 53%.
    Absorber design removal  efficiency; overall  removal efficiency  is 71%.

-------
       TABLE 4-3.   S02  REMOVAL EFFICIENCIES:   CONTINUOUS MONITORING DATA
Uti lity name/
unit name
Colorado Ute
Craig 2



Kansas City Power &
Light
LaCygne 1
Kansas Power & Light
Lawrence 4

Louisville G&E
Cane Run 4




Cane Run 5
Cane Run 6
Mill Creek 3
Montana Power
Colstrip 1



Northern Indiana Public
Service
D.H. Mitchell 11


Northern States Power
Sherburne 2


Pennsylvania Power
Bruce Mansfield 1
Philadelphia Electric
Eddystone 1A
South Carolina Public
Service
Winyah 2

South Mississippi
R.O. Morrow, SR, 1



R.O. Morrow, SR. 2




Unit rating,
MW (gross)

455





874

125


188




200
288
442

360





115



740



917

120


280


200



200




Process
type

Limestone





Limestone

Limestone


Lime




Lime
Dual alkali
Lime

Lime/alkaline
flyash




Wellman Lord



Limestone/
alkaline
flyash

Lime

Magnesium
oxide

Limestone


Limestone



Limestone




Fuel
sulfur
content,
%

0.5





5.4

0.6


3.8




3.8
4.8
3.8

0.8





3.5



0.8



3.0

2.6


1.7


1.3



1.3




Design removal
efficiency, %

85





80

73


85




85
95
85

60





90



50



92

90


69


85a



a
85




Date

5/80
6/80
7/80
8/80


9/77

10/77
2/79

7/77
8/77
10/77
11/77
7/80
7/80
6/80
6/80

4/76
7/76
9/76
12/76


8/77
10/77
Actual removal
efficiency, %

65
66
66
66


81

97
94

81
84
84
84
87
85
95
85

86
90
89
81


90
90
11/77 ; 91

4/77



10/77

9/77
11/77

6/79
7/79
8/79
4/80
5/80
6/80
7/80
8/80
9/79
5/80
6/80
7/80
8/80

58



81

97
85

80
84
80
80
80
90
90
80
95
85
90
85
80
(continued)
                                      154

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TABLE 4-3  (continued)
Utility name/
unit name
Tennessee Valley Author'
Widows Creek 8

























Unit rating,
MW (gross)
ty
516

























Process
type

Limestone

























Fuel
sulfur
content,
%

3.7

























Design- removal
efficiency, %

89

























Date

11/77
12/77
1/78
2/78
3/78
4/78
5/78
6/78
7/78
8/78
9/78
5/79
6/79
7/79
8/79
9/79
10/79
11/79
12/79
1/80
2/80
3/80
4/80
5/80
6/80
7/80
Actual removal
efficiency, %

91
94
89
85
92
90
89
92
88
89
91
80
84
86
88
83
87
88
86
84
84
83
86
83
82
87
    a Absorber design removal efficiency; overall  removal efficiency is 53%.
                                                  155

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limestone installations.   The  two exceptions  are demonstration
systems  utilizing  dual  alkali and  magnesium  oxide processes.
The available data,  although not extensive, indicate that actual
removal  efficiencies  of these systems  generally meet or exceed
design values  at both  low-sulfur and  high-sulfur  coal instal-
lations.   This would  seem  to indicate that meeting or exceeding
design S02 removal efficiency has not been a significant problem
for FGD  systems  on  units firing high-sulfur coal.  For example,
the FGD  installation at the La  Cygne  power  station  (the FGD-
equipped unit currently firing the highest-sulfur coal) success-
fully passed performance testing early in 1975.  Results from 10
days of  continuous  monitoring in  late  September 1977 indicated
that  the system was continuing  to  exceed  its  design removal
efficiency of 80%.


PERFORMANCE CONSIDERATIONS

     Because of  the  widely varying conditions at stations where
FGD systems  are applied (e.g., differences  in plant size, coal
sulfur content,  and required removal efficiencies),  it is dif-
ficult  to  pinpoint  specific  variables  affecting  overall  FGD
system  performance.   Certain  general  considerations  can  be
identified, however, and are discussed below.

S02 Inlet Levels and Removal Requirements

     In  general, FGD systems  operating on  units  with  low to
medium  S02   inlet  levels  have  demonstrated  a higher  level of
overall  dependability than those  operating on units with higher
inlet  levels.   This is  illustrated  in  the statistical analyses
of  the  overall  FGD system  availability  (Figure 4-8)  for low-
sulfur coal units.  Obviously, the lower SO2 removal requirement
contributes to this difference.

Unit Load Profile and Coal Characteristics

     Higher  dependabilities have  resulted from  a  reduction in
the number  of chemical  and mechanical  problems  on FGD systems
applied  to  new,  base-loaded boilers  designed to fire coal  from
one or several specific  sources.  The flue gas generated by  such
units  generally  has  more relatively constant  and stable charac-
teristics, and  overall  system dependability apparently improves
because  the  system does not have  to respond to dramatic varia-
tions  in flue gas  flow rates and composition.   In FGD systems
retrofitted to cycling,   and peak-load units, these  systems often
must respond to conditions  that  reach or  exceed their process
control  capabilities,  and  problems  result  from the variations
that occur  in reagent  feed rate and loss of chemical control.
                                156

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System Redundancy and Bypass Capability

     FGD systems  are  now  considered  an  integral  part  of the
power generating plant,  and more  stringent regulations prevent
many utilities from bypassing the FGD system.  Thus, the current
design trend  is  toward incorporation  of  spare  absorber modules
and  ancillary  equipment.    Systems  so  designed  have  greater
dependability because the failure of a single component does not
necessarily  force  the entire  system off  line.   Spare capacity
also promotes a more flexible operating and maintenance strategy
by  allowing  some  routine  maintenance to  be performed without
removing the system  from  service.   The  result  is  an overall
reduction in FGD system downtime.

Utility Experience

     As  utilities   continue to  gain  more experience  with FGD
system  operation,  overall  system dependabilities  are expected
rise.  In the  early stages of FGD operation, utility staffs had
little  experience  with the chemical processes involved  in FGD
operation,   and the  chemical and  mechanical problems  that are
inevitable with  complex processes such  as these  were difficult
to  rectify.   The steadily increasing commercial operating hours
will  allow  system  operators and maintenance personnel  to gain
the  experience  necessary  for  more  efficient and expeditious
analysis of system problems  and implementation of solutions.  In
addition, utilities are  employing more chemical  engineers and
other  personnel  familiar  with  gas/liquid  systems  to  deal with
these problems.

Operating and Maintenance Philosophy

     A general trend in plant philosophy regarding  operation and
maintenance  (O&M)  is  the  dedication of specific crews to handle
this  responsibility,  rather  than considering  it  a   secondary
function of the power plant  O&M personnel.   This change will
permit  faster  and  more precise changing of system  parameters to
meet  varying  load conditions,  and  overall  system reliability
should improve as problems  are attended to expeditiously.

System Design Generation

     Building  on experience  gained  in the operation of  first-
generation  systems,  system  suppliers  and  designers are now
providing better process  design configurations and  materials of
construction.  Indicative  of this trend are  the broader  guaran-
tees  system  suppliers  are  now  offering   with  respect  to S02
removal  efficiency,   mist  carryover,  waste  stream  quality/
quantity, power consumption, reagent consumption, and  availabil-
ity.   Many  of  the newer  systems should  exhibit  fewer  of the
traditional  operating  problems,  especially during  the critical
startup and debugging phases of operation.
                                157

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                            SECTION 5

                    CAPITAL AND ANNUAL COSTS
INTRODUCTION

     Another important function of the utility survey program is
the  acquisition  and  analysis  of  cost  data.   In  this program,
emphasis is on costs associated with operational systems because
of the availability of meaningful and complete data.  These data
are adjusted only  to  ensure  their completeness and accuracy and
to facilitate comparison.  The  approach and methodology used in
analyzing  these  costs  and  the  results  of these  analyses are
briefly described in the following subsections.


APPROACH

     Capital and  annual cost  data  on  operational  FGD systems
have  been  obtained continuously since March 1978.   Costs for
each  system  are  obtained directly  from the  utilities  and from
published  sources,  and  then  itemized  by  individual  FGD cost
element.  The itemized costs are then adjusted to a common basis
to enhance comparability.  This  adjustment includes factors for
estimating costs not  given by the  utilities  and escalating all
costs to common dollars  (mid-1980).  All adjusted cost data and
computations  are   reviewed   and  verified  with  the  appropriate
utility.

     It is  important  to note  that the costs analyzed here are
real  costs,  not   cost  model  projections.   When  a  particular
itemized cost is not  reported  by the utility, an estimated cost
based on known system design and operating factors is included.
The use of  estimates  is not arbitrary; they  are used only when
cost items are unavailable or are judged to be unrepresentative.


ADJUSTMENT PROCEDURE

Capital Costs

          All  costs  associated  with  control  of  particulate
          matter emissions are deducted.
                                158

-------
         Capital   costs   for   modifications  necessitated   by
         installation  of an FGD  system are added if  they were
         not  included  in the reported  costs.

         Sludge'disposal  costs  are adjusted  to  reflect a  20-
         year life  span for retrofit systems  and  a 30-year life
         span for new  systems.

         Any  unreported direct and  indirect  costs incurred  are
         estimated  and included.

         All  capital  costs are  escalated to  mid-1980 dollars.

         All  $/kW values reflect the  gross  generating capacity
         of the  unit.
Annual Costs
          All  costs  are  adjusted to  a  common  65%  capacity
          factor.

          Direct costs that were not  reported are estimated and
          added.

          Overhead  and  fixed costs that  were not  reported are
          estimated and added.

          All  annual  costs are  escalated to  mid-1980  dollars.

          All  mills/kWh values  are  based  on  a 65%  capacity
          factor  and  the net generating  capacity of the  unit.
RESULTS
     Table 5-1  summarizes  both reported  and  adjusted costs for
all 45 operational FGD systems on which cost data were obtained.
This  table  also  summarizes  the  results  by  application  (new/
retrofit) and  by  sulfur  content of  the coal  (high sulfur/low
sulfur).  Table  5-2   lists  the  results  by  process type.   A
plant-by-plant  listing of the  reported and  adjusted costs for
the operational FGD systems  addressed in this study is provided
in Appendix  B.


COST MODEL COMPARISON

     During   the  past  few  years,  various  organizations  have
conducted major cost  studies  of the capital and  annual  costs
associated with different FGD processes.  Reasons for these cost
studies range from comparing the economics associated with
                                159

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                           TABLE 5-1.  CATEGORICAL RESULTS OF THE REPORTED AND ADJUSTED
                               CAPITAL AND ANNUAL COSTS FOR OPERATIONAL FGD SYSTEMS
Results
All
New
Retrofitted
High sulfur
Low sulfur
Reported
Capital
Range,
($/kW)
23.7-174.8
23.7-174.8
29.3-157.4
29.3-157.4
23.7-174 8
Average,
($/kW)
78.9
78.4
79.6
75.1
82.3
Annual
Range,
(mills/kWh)
0.29-13.02
0.29- 5.81
0.46-13.02
0.92-13.02
0.29-11.32
Average,
(mills/kWh)
2.97
2.19
4.54
3.71
2.09
Adjusted
Capital
Range,
($/kW)
35.1-258.9
35.1-242.1
57.5-258.9
57.5-233.6
35.1-258.9
Average,
($/kW)
116.2
107.4
131.4
106.3
122.6
Annual
Range,
(mills/kWh)
1.80-18.64
1.80-13.44
4.36-18.64
3.70-18.37
1.80-18.64
Average,
(mills/kWh)
7.64
6.49
9.38
7.48
7.40
(Ti
O

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TABLE 5-2. ADJUSTED CAPITAL AND ANNUAL COSTS FOR OPERATIONAL
              FGD SYSTEMS BY PROCESS TYPE
Process
Limestone
Lime
Dual alkali
Lime/
alkaline
flyash
Sodium
carbonate
Wellman-
Lord
Limestone/
alkaline
flyash
Reported
Capital
Range
(J/kW)
23.7-168.0
29. 3-122. 8
47.2-174.8
92.5-101.4
42.9-113.6
132. 8-1 57- 4

Average
($/kH)
68.8
71.0
97.8
98.4
72.4
142.4
49.3
Annual
Range
(mills/kWh)
0.29- 7.80
0.92-11.32

1.25- 2.97
0.23- 0.46


Average
(mills/kUh)
2.47
3.69
1.30
2.40
0.38
13.02
0.75
Adjusted
Capital
Range
($/kH)
35.1-148.7
57.5-192.7
80.6-242.1
131.0-133.8
79.9-138.5
233.6-258.9

Average
($/kW)
99.6
104.5
134.6
132.9
101.7
249.1
94.5
Amu
Range
(mills/kWh)
1.80- 8.56
3.70-10.82
5.10-13.44
5.99- 7.79
5.29- 6.78
1.7.86-1.8.37

al
Average
(mills/kWh)
6.02
6.91
8.11
7.19
6.02
. V8.10
4.63

-------
commercial  and emerging  FGD  processes to  determining the  cost
impact  of  increasingly  stringent  S02   standards.    Table  5-3
presents  the  results  of several  representative  cost  studies
recently completed  and  the  assumptions on which they  are based.

     In this  table, the  capital  and annual  cost  estimates  and
their  underlying assumptions  are  summarized  for  a  number of
"base  cases."   In  this context,  "base  case" refers  to  a  con-
ventional wet limestone slurry FGD process such as that  typical-
ly  installed on  a  new 500-MW  (net) boiler  firing high  sulfur
eastern coal.   This table shows  that capital  and annual  costs
vary  widely,  with  the  capital  values  ranging  from  $94.5 to
$194.4/kW  and  the  annual  values   ranging  from  4.03  to  16.91
mills/kWh.   These wide variations  in  estimated costs  for  es-
sentially the same case result from  differences in the intent of
the studies and in the assumptions on which each is based.   With
respect to  the  latter,  variations  can be noted  for virtually
every key assumption.

     By use of the  reported  and  adjusted capital  and  annual
costs  for  the operational FGD systems  presented in Appendix B,
it  was possible  to compare the  estimated costs  in these  cost
studies with actual  costs.   For  this comparison, only limestone
systems have been analyzed,  as this was  the  "base case"  of  all
the aforementioned cost studies.

     Table 5-4 presents the adjusted capital and annual costs of
the limestone systems currently in service on coal-fired  utility
boilers.   Generally,  these  costs  represent  the  technology of
first-generation  limestone  systems  that  have  been operational
for  several years.   Many  have  bypass  capabilities.   Most of
these systems scrub less than 100% of the flue gas and therefore
do  not require a separate reheat  system.   A significant  number
of  units have  total removal  efficiencies of less than 70%.   Few
systems have spare  components  and  few have oversized components
to  provide  spare capacity.   Sludge  is  typically disposed of in
ponds without fixation or treatment.

     A comparison shows that  capital and annual costs of actual
systems approach the costs  developed  by the  Tennessee  Valley
Authority  (TVA)  and Beychok  cost  studies.   The  actual  average
capital cost for  limestone  FGD  systems  is  $99.6/kW;   average
annual cost is  6.03  mills/kWh.   The TVA cost study arrived  at a
capital cost  of $97.5/kW and an annual cost  of 4.03 mills/kWh;
the Beychok cost study,  a capital cost of $94.5/kW and an annual
cost of  6.61 mills/kWh.   The criteria  used  in  developing  the
costs  in  these two  studies  are also  based on early  FGD  tech-
nology.

     Assumptions used in  the  other cost studies reflect  future,
more advanced  FGD system designs.   They  also reflect inclusion
                                162

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                                       TABLE  5-3.    BASE  CASE  CAPITAL AND  ANNUAL  COST  ESTIMATES
01
Category
General criteria:
Sponsoring organization
Year prepared
Plant size
Plant location
Plant capacity, HW (net)
Plant capacity factor, i
Plant application
Plant heat rate, Btu/kWh (net)
Fuel (source) ;
Fuel characteristics, HV/S1/AJ
Emission standard ,
SO? emissions, lb/10 Btu
S02 removal efficiency, X
Process design criteria:
Process
Number of modules
Number of spares
Gas bypass capability
Reheat AT, °F
Water loop
Solids dewatering, X solids
Sludge treatment
Sludge disposal
Economic criteria:
Capital cost basis
Annual cost basis

Battery limits

Price level

Cost estimates:
Total capital cost, $/kW
Total first year annual costs,
mills/kWh
FGD economic studies
3
Bechtel

EPRI
1979
2-unit
North Central
1000
70
New
9986
Coal (Illinois)
10.100/4.0/16.0
Revised NSPSa
1.2
87

Limestone
8
2
Complete bypass
56
Closed
50
Fly ash/lime
Truck/landfill

Total
Total first
year revenues
Gas inlet to
sludge disposal
July 1978


157.3
8.9

PEDCo 4
Environmental

EPA
1977
1-unit
Midwest
500
65
New
9000
Coal (Eastern)
12,000/3.5/14.0
Revised NSPSb
0.6
90

Limestone
5
1
Complete bypass
50
Closed
50
Fly ash/lime
Pumping/ pond

Total
Total first
year revenues
Gas inlet to
sludge disposal
July 1980


160.2
10.5

5
Steams-Roger

EPRI
1979
1-unit
North Central
500
70
New
9724
Coal (Illinois)
10,100/4.0/16.0
Revised NSPSC
0.8
90

Limestone
4
1
Complete bypass
50
Closed
45
Fly ash/lime
Truck/landfill

Total
Total first
year revenues
Gas inlet to
sludge disposal
July 1978


179.7
7.86

Beychok/ (
Stone & Webster

EPRI
1977 to 1978
1-unit
Midwest
500
70
New
9000
Coal (Eastern)
12,000/3. 5/NA
Revised NSPSd
0.5
90

Limestone
HA
MA
NA
Yes
Closed
Yes
Fly ash/line
NA

Total
Total first
year revenues
Gas inlet to
sludge disposal
First quarter 1977


94.5
6.61

7
SRI/Radlan

EPR!
1979 to 1980
1-unit
NA
499
70
New
NA
Coal (Eastern)
10.100/4.0/16.0
Revised NSPS6
0.5
93

Limestone
5
1
Complete bypass
50
Closed
60
Fly ash/lime
Truck/ landfill

Total
Total first
year revenues
Gas inlet to
sludge disposal
January 1979


194.4
16.91

8
TVA

EPA
1979
1-unit
Midwest
500
80
New
9000
Coal (Eastern)
10.500/3.5/16
NSPSf
1.2
80

Lines tone
4
0
No bypass
50
Closed
None
None
Pumping/ pond

Total
Total first
year revenues
Gas inlet to
sludge disposal
Mid-1979 (capital)
Mid-1980 (annual)

97.5
4.03

NA = Not available.
'Proposed standard of September 1978.
 Evaluated sti"d?rds in anticipation of revision to  NSPS.
Promulgated st ajlgited NSf 3
                    sled standard as stringent e?
              efcvalui'-cj standards more string--/
               Pre--'1- -•
                            <"i ol 1971 .

-------
             TABLE  5-4.   ADJUSTED  CAPITAL  AND  ANNUAL COSTS OF
                      OPERATIONAL  LIMESTONE  FGD SYSTEMS
Utility name
unit name
Alabama Electric Coop
Tombigbee 2 and 3
Arizona Public Service
Choi! a 1
Choi la 2
Central Illinois Light
Duck Creek 1
Indianapolis Power & Light
Petersburg 3
Kansas City Power & Light
LaCygne 1
South Carolina Public Service
Winyah 2
South Mississippi Electric Power
R.D. Morrow, SR. 1 and 2
Southern Illinois Power Coop
Marion 4
Springfield City Utilities
Southwest 1
Tennessee Valley Authority
Widows Creek 8
Average

$/kW, capital

35.1

74.6
148.7

121.3

148.4

81.4

43.1

108.7

110.8

133.5

145.1
99.6

mills/kWh, annual

2.91

4.36
7.64

7.96

8.59

6.89

1.80

6.01

7.12

7.66

8.56
6.03
The variability of these figures occurs in part because FGD systems in-
stalled on some boilers do not accommodate 100% of the boiler flue gas.
The costs for such systems are proportionately lower than those for full
capacity FGD systems.   This is magnified by the conventional use of gross
kW for the $/kW figure and net kW for the mills/kWh figure, regardless of
the % of the flue gas  scrubbed.   These figures represent -the capital and
annual costs required  to bring the individual  units into compliance.
                                    164

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of a separate  reheat system,  the effects of  more  stringent S02
emission standards,  more  elaborate sludge  disposal  strategies,
and one spare scrubber module for extra capacity.
                                165

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                            SECTION 6

                           CONCLUSIONS


     The  discussion in  the  preceding sections  of  this paper
indicates that  the  significant rate  of growth observed in the
development  and application  of FGD  technology  for coal-fired
utility  boilers  has been  matched  by  the  considerable  improve-
ments  observed  in  the performance of  the  operational  systems.
With respect to the latter,  the most significant improvement in
the  performance of the  operational   systems  involves  the  in-
creased level of dependability observed for the high sulfur coal
units.   During  the  past  2  years, the dependability  of these
systems  has  improved to a level which approaches that  observed
for  the  low sulfur coal  units.   It  is  anticipated  that this
trend will  continue and will  be  reflected in  less startup and
commercial  operating problems  for  systems  now being  placed in
service or planned for service.

     Promoted by the requirements set forth in the Clean Air Act
Amendments and the  pursuant  NSPS,  application of FGD to all new
coal-fired  utility  boilers  constructed in the  near  future  is
anticipated.
                                166

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                          REFERENCES
1.   U.S. Department of Energy.  Energy  Information Administra-
    tion.   Office   of Coal   and  Electric   Power  Statistics.
    Electric  Power  Statistics Division.   Inventory  of  Power
    Plants  in  the  United  States,  December  1979.   Publ.  No.
    DOE/EIA-0095(79).

2.   Rittenhouse,  R. C.  New Generating  Capacity:  When,  Where,
    and  By Whom.   Power Engineering  82(4):57,  April 1978.

3.   Bechtel  National,  Inc.    Economic  and  Design  Factors  for
    Flue Gas Desulfurization  Technology.   EPRI CS-1428,  April
    1980.

4.   PEDCo  Environmental,  Inc.  Particulate  and Sulfur  Dioxide
    Emission   Control  Costs  for   Large  Coal-Fired   Boilers.
    EPA-450/3-78-007 (NTIS PB 281271),  February 1978.

5.   Augustine,  F.,  S.  D.  Severson,  and  J.  L.  Winter.   Economics
    of Four  FGD Systems.  Prepared  for  Electric Power Research
     Institute  by  Stearns-Roger Engineering Corporation  under
    EPRI Research  Project  No. 1180-3,  Draft  Report,  November
     1979.

6.   Beychok,  M. R.  Comparative Economics of Advanced Regener-
     able Flue  Gas  Desulfurization Processes.   EPRI  CS-1381,
    March  1980.

7.   Oliver,  E.  D.   and  K.  Semrau.   Investigation  of High  SO?
    Removal  Design  and  Economics,  Volume 2:   Economics.   EPRI
     CS-1439,  June 1980.

8.   Tomlinson,  S. V-, F. M.  Kennedy,  F. A.   Sudhoff,  and R.  L.
    Torstrick.    Definitive   SO   Control  Process  Evaluations:
    Limestone,   Double-Alkali,  and  Citrate   FGD   Processes.
    EPA-600/7-79-177 (NTIS PB 80-105828),  August 1979.
                                167

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                           APPENDIX A

           FLUE GAS DESULFURIZATION INFORMATION SYSTEM
BACKGROUND

     The  most  significant product  of EPA's utility FGD survey
program is a quarterly summary report generated from a computer-
ized data base known as the Flue Gas Desulfurization Information
System  (FGDIS).   This  data base  represents  the latest develop-
ment  in this program.   Previously,  manually updated  and semi-
automated data  files  were used  to  store and  retrieve informa-
tion.  The increased emphasis  on FGD for SO2 control  (resulting
from  its  commercial  development) necessitated  a more efficient
data  storage/retrieval  system  for  processing  and transmitting
these data.   In the fall  of  1978,  FGDIS was  developed to meet
this need.
DESCRIPTION

     Design  and  performance data  for both  the  operational and
planned domestic  utility FGD systems  are stored  in the FGDIS.
Also stored  are  data on operational  domestic scrubbers for re-
moval of particulate matter  and data on operational FGD systems
applied to coal-fired utility boilers in Japan.

     The design  data contained in  FGDIS encompass  the entire
emission control  system and the power-generating unit to which
it is applied.  Descriptions  include location, standards limit-
ing  emissions  of  S02  and particulate  matter, power-generating
capacity,  boiler  and stack information,  average fuel  analyses,
and  other  more general  data.   Input  of design data specific to
FGD  systems  ranges  from  general   information such  as process
type, system  supplier,  and initial  system startup date to more
specific component  design  information  and operating parameters
such as absorber  type,  gas and liquid  flow rates, and pressure
drop.  Also included in the data are descriptions of the methods
of solids  concentrating and waste disposal,  flue gas reheat, and
mist elimination,  and  information  on capital costs and annual
revenue requirements of FGD systems.

     For operational FGD systems,  the FGDIS  stores comprehensive
performance  data,  including  periodic  dependability parameters
                                158

-------
and the service  times (operating,  forced-outage,  and scheduled
outage)  from which they are calculated.   Where available, actual
system  S02   and  particulate  matter  removal  efficiencies  are
included  (and  qualified).   Problems  encountered  with  system
operation  and  solutions implemented  to correct  them  are  des-
cribed.  The performance of the FGD-equipped boiler is described
in terms of  service time,  production (kWh),  and capacity factor.

     Figure   A-l  presents  a  complete  FGDIS  structure  diagram
illustrating all of the information  areas  and some  of the key
data entries contained in the system, as well  as  the hierarchy
associated with them in the data base.  General unit data are at
level 0,  whereas most of the  specific component  data  are  at
Level 3.
CAPABILITIES

     In addition to  being used to generate  a quarterly report,
FGDIS  is  also available  for direct  on-line access.   This im-
portant function  not only provides  interested parties  with an
opportunity to examine data that are too specific for convenient
inclusion in the quarterly report,  but it also provides immedi-
ate access  to  information that has been  loaded  into the system
but not yet published  (i.e.,  information that has become avail-
able during the period  between  quarterly reports).  Information
is gathered,  reduced,  verified,  and loaded  into  the FGDIS on a
continual  basis  to  ensure that  the  files  remain  current and
complete.

     Access to the  FGDIS data  files  and -manipulation  of these
data are accomplished via MRI  System 2000 .   This comprehensive
data  base  management   system  offers  extensive   data  retrieval
capabilities.   The  set of  user-oriented commands  provided are
flexible enough to satisfy virtually  any information need.  The
PRINT  command  will  produce the compilation  of  a simple sequen-
tial  list,  or a set of report writer commands  will  produce a
tabulation  of the   requested  data  in  a predetermined report
format.   Utilization  of  system  functions   (average,   standard
deviation,  summation, maximum value,  minimum value) will elicit
statistical analyses of the  numerical  data in  the files.  In
addition,  the data requested  through  the available  commands can
be selectively  limited by  a set  of  criteria  included in the
commands.    This  feature  facilitates  examination of  design or
performance parameters for a specific unit or a specific process
type,   and  so  on.   The  retrieval possibilities  are limited only
by the needs and imagination of the user.

     The  FGDIS files   are  stored  at  EPA's National   Computer
Center (NCC) in Research Triangle  Park, North Carolina, and are
accessible via a nationwide communications network consisting of
                                169

-------
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  QUEhCHEH/
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QUENCHER TYPE
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  AJSORBEBS

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LOCATION
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                                                                                                REAGENT
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   TANKS

TANK TYPE
LOCATION
CONFIGURATION
CAPACITY
   PU»S

F-IW TYPE
MANUFACTURER
CAPACITY
SERVICE
                                                                                                                                     COII
                                                                                                             SOL IDS
                                                                                                            ICENTRATl
 DEUAIER1NG
DEVICE TYPE
CAPACITY
INLET SOLIDS
XJTLET SOLIDS
                                                                                                                                                   END PRODUCT
                                                                                                                                     RECOVERABLE
                                                                                                                                       PRODUCT

                                                                                                                                     TYPE
                                                                                                                                     CJJANTITY
                                                                                                                                     DT5POSTTIOH
                                                                                                                                                              INSTHUHENTMfOH
                                                                                                           -CHEH1CA1.
                                                                                                           •PHYSICAL
WATER BALANCE

WATER LOSSES
WATER AOD,
WATER SOURCE
POINTS OF AOD,
                                                                                                                       CHEN. FUNCTION
                                                                                                                       CHEH. NAPE
                                                                                                                       CONSOHPTION
                                                                                                                                                                                                           cn»t«
                                                                                                                                                     moncn
                                                                                                                                                    joiuuaa
                                                                                                                                                                                                                                      FUCBIEII
                                                                                                                                       SLUDGE
                                                                                                                                      QUANTITY
                                                                                                                                      COMPOSITION
I
TREATHEHT
METHOD
DEVICE TYPE
INLET CHAR.
OUTLET CHAfl,

DISPOSAL
INTEftlK/FIKAL
im
LOCATION
SITE CAPACITY
                                                                                  Figure  A-l.     FGDIS   structure   diagram.

-------
local  telephone  numbers  in   21   cities  and  WATS  services.
Arrangements are currently being made so that persons interested
in gaining  access  to  the  FGDIS  can  obtain  account  numbers,
training,  and additional information from the National Technical
Information  Service (NTIS), Springfield,  Virginia,   in addition
to providing continual  on-line  access  capability,  NTIS also can
process selective  information  requests for  limited information
needs that  do  not warrant acquisition of. ,a  permanent computer
account number  (single  requests  for specific tabulated informa-
tion).
                                171

-------
                                    APPENDIX  B

                REPORTED AND ADJUSTED CAPITAL AND ANNUAL COSTS  FOR
                              OPERATIONAL  FGD SYSTEMS

Alabama Electric
Tcmbigbee 2
Tonbigbee 3
Arizona Public Service
Choi la 1
ChollJ 2
Central Illinois light
Duck Creek 1
Central Illinois Public Service
Newton 1
Columbus i. Southern Ohio Electric
Conesville 5
Conesville 6
Ouquesne Light
El rang 1-4
Phillips 1-6
Indianapolis Power » Light
Petersburg 3
Kansas City Power t Light
Hawthorn 3
Hawthorn 4
LaCygne 1
tofttuckv Utilities
Sreen River 1-3
Louisville Gas t Electric
Cane Run 4
Cane Run 5
Cane Run 6
Hill Creek 3
Paddy's Run 6
Mlnnkota Power Cooperative
Hilton R. Young 2
Monongahela Power
Pleasants 1
Montana Power
Col strip 1
Col strip 2
Nevada Power
Reid Gardner 1
Reid Gardner 2
Reid Gardner 3
Northern Indiana Public Service
Dean H. Mitchell 11
Northern States Power
Sherburne 1
Sherburne 2
Pacific Power I Light
Jim Bridger 4
Pennsylvania Power
Bruce Mansfield 1
Bruce Mansfield 2
Philadelphia Electric
Eddys tone 1
Public Service Company of New
Mexico
San Juan 1
San Juan 2
South Carolina Public Service
Authority
Winyah 2
South Mississippi Electric
R.D. Morrow 1
R.O. Morrow 2
Southern Illinois Power Coop
Marion 4
Southern Indiana Gas * Electric
A.B. Brown 1
Springfield City Utilities
Southwest 1
Tennessee Valley Authority
Widows Creek B
Utah Power I Light
Hunter 1
Huntington 1
	 KB
Capital cost
6,992.100
6.992,100
6,550,000
44,352.000
30.583,000
107,831,000
22,836,000
22,836.000
59,541,000
50,356,000
55,724,000
3,220,000
3.220,000
46,900.000

4,500.000

12.647,000
12.481,000
20.596.900
18,846,880
3,700,000

44,119,500

65,693,400

36,500,000
36,500.000

5,363.378
5,363,378
14,200.565

18.192,040

34,982,000
34,982,000

49,643,000

110,639,000
110.639,000

30.856,000


47,944,410
47,985,000


6,646,000

10.896,000
10,696,000

15,200,930
12,495,000
16,744,500
47.900,000
24.400,000
27.090,000
Total/kW
27.4
27.4
52.0
168.0
73.5
174.6
55.6
55.6
116.8
122.8
99.5
29.3
29.3
53.7

70.3

66.6
62.4
71.5
42.6
52.9

92.5

106.3

101.4
101.4

42.9
42.9
113.6

157.4

49.3
49.3

90.3

120.6
120.6

285.7


132.8
137.1


23.7

53.7
53.7

87.9
47.2
86.3
87.1
56.7
63.0
oorted
Annual
217,464
217,464
NA
1.003,568
10,851,000
NA
9,132,726
9,132.726
21,027.000
18,301,000
NA
346,441
M6.441
7,413,047

364,005

960.301
763.443
NA
321 ,463
N«

1.779,375

9,015,879

6,128,000
6,128,000

251,514
251,514
131,824

2,414,589

2,716,758
2,716,758

NA

9,979,850
9,979,850

3,808,000


NA
NA


527,000

NA
NA

859,453
1,850,565
778,749
14,576,400
OA
2,946,400
Mills/kWh
0.33
0.33
NA
0.75
5.54
NA
5.81
5.81
7.18
11.32
NA
1.15
1.15
4.99

5.20

1.29
0.92
NA
1.25
NA

1.25

2.73

2.97
2.97

0.46
0.46
0.23

13.02

0.75
0.75

NA

3.28
3.28

6.37


NA
NA


0.29

NA
NA

1.03
1.30
1.20
7.80
NA
1.27

Capital
8,949,850
8,949,850
9,400,764
39,748,800
50,452,200
149,388,600
76.423,700
76,423,700
87,852,700
78,993,100
78,967,000
6,329,500
6,329,500
71.124,100

7.682,400

20.045,000
17,146,000
23,205,000
26,751,200
7,288,000

62,872,500

70,058,000

48,183,500
48,183,500

9,992,150
9,992,150
17,307,000

26,999,900

67,996,450
67,996,450

59,732,500

121,270,800
121,270.800 .

20,206,400


92,034,400
90,608,200


12,060,300

22,056,750
22,056,750

19.177,750
21,477,900
25,904.900
79,785,300
29,625,000
Adjusted
i/kW
35.1
35.1
74.6
148.7
121.3
242.1
93.0
93.0
172.3
192.7
148.4
57.5
57.5
81.4

120.0

105.5
85.7
80.6
60.5
104.1

131.0

113.4

133.8
133.8

79.9
79.9
138.5

233.6

94.4
94.4

108.6

132.3
132.3

187.1


254.9
258.9


43.1

108.7
108.7

110.8
81.1
133.5
145.1
68.9

Annual
3,893,050
3,893,050
3,130,900
10.221,000
17,143,200
44,003,900
26,288,970
28,288,970
30,006,600
35,558,600
25,189.600
2,436,200
2.436,200
32,189,700

2,817.900

5,334,000 '
4.975,500
8,867,600
8,855,500
3,746,200

13,914,300

26,148,300

14,719,250
14,719,250

3.314,600
3,314,600
4,247,300

9,832,000

18,990,800
18,990,800

19,440,100

44,890,750
44,890,750

6,296,400


31,930,100
31,483,100


2,648,100

6,162,250
6,162,250

6,525,600
7,252,100

^Hills/Mi
2.91
2.91
4.36
7.6S
7.96
13.44
6.62
6.62
10.82
18.64
8.59
4.39
4.39
6.89

8.25

5.15
4.56
5.79
3.70
10.36

5.99

7.92

7.79
7.79

5.29
5.29
6.78

18.37

4.63
4.63

6.71

9.5c
9.56

•,0.5j


. 17.86
18.07


1.80

6.01
6.01

7.12
5.13
7,413,800 7.66
25,140.300
9,492,200
8. 56
4.17
5.28
NA » Not available.
                                         '172

-------
                        The  Department  of Energy's

                          Flue  Gas  Desulfurization

                      Research  and  Development Program

                          Edward C. Trexler,  P.  E.
                        U. S.  Department  of  Energy
                        Office of  Coal  Utilization

The Department of Energy's flue gas desulfurization  (FGD)  research  and
development activities are conducted as  part  of the  Advanced Environmental
Control  Technology Program (AECT) which  is managed within  the organization
of the Assistant Secretary for  Fossil  Energy.  This  new  AECT program was
initiated in FY 1979  with  a goal  to identify, research,  develop,  refine and
demonstrate cleanup equipment that  will  clean flue gas for compliance with
existing and anticipated environmental pollution regulations, and equipment
that will remove the  undesirable components from coal  derived gas streams
to assure reasonable  life  for utilization  equipment  such as  gas turbines
and fuel cells.  The  flue  gas cleanup portion of the AECT  program budget
amounted to $2.7 million in FY  1979 and  $20.1  million  in FY  1980.

The FGD project is divided into two parallel  efforts identified by  the  sched-
uled completion dates as very near-term  (end  1983) and near-term  (end 1986).
The very near-term effort  aims  at improving the SC^  removal  efficiency  and
reducing the waste disposal problems of  conventional lime/limestone scrubbers,
This is being done in coordination  with  EPRI  and EPA scrubber improvement
programs, through private  sector scrubber  instrumentation  and analysis, by
tests at TVA and other utility  prototype and  full-scale  scrubber  facilities,
and by transfer of process improvement information.  The near-term  effort is
aimed at supporting newer  technology S02 removal processes that include non-
regenerable (throwaway) and regenerable  systems  that produce potentially
marketable by-products such as  sulfur and  sulfuric acid.  These technologies
are, or will, be under experimental  test at Fossil Energy  Technology Centers,
under prototype testing by DOE  and  EPRI  at TVA and other sites, and under
initial  commercial use evaluation by DOE at power stations and industrial
plants.   As these technologies  mature, private industry  will be encouraged
to cost-share development  with  the  Government.   Information  on progress will
be disseminated via reports,  symposia, plant  visitations,  demonstrations
and workshops.
                                     173

-------
                         The Department of Energy's
                          Flue Gas Desulfurization
                      Research and Development Program

NATIONAL PRIORITIES IN ENERGY AND ENVIRONMENT

The Nation's entrance into the 1980's is characterized by the need to
solve difficult and interrelated problems.  High on this priority list
are the needs to significantly reduce oil  imports, to protect and enhance
the environment, and to improve the economic posture of the Nation through
increased national  productivity.  That these needs are important to the
Nation is evidenced by the abundance of contemporary legislative activity
which promotes both the diminished use of oil and gas through coal utili-
zation and the enhancement of the environment.   Explicit in these legis-
lative acts is the need for achieving these goals within the bounds of
economic constraint.  Meeting these goals  will  require the coordinated
effort of both the private and public sector.  This paper seeks to pro-
mote such coordinated effort by presenting the Department of Energy's Flue
Gas Desulfurization Research and Development Plans.  It is our desire that
this summary serve as a focal point for new and improved communication, and
that the end result will be success through a better coordinated effort.

The approach in this paper is to identify  the energy challenge in terms of
flue gas desulfurization system needs, to  introduce you to our new cleanup
technology efforts  and how the FGD program is oriented to other DOE pro-
grams, to'note our special relationships with EPA, TVA and EPRI, and to
discuss in some detail particular programs which we are pursuing.  In
addition, we would also have you join with us in examining the challenges
and opportunities of the future.

THE ENERGY CHALLENGE

The oil importation reduction challenge perhaps can be best appreciated by
observing our recent energy flow from supply through consumption, and by .
comparing consumption with domestic supply.  Domestic and imported supply^
in 1977 was:

                   Supply                      Quads/Yr.

               Domestic Coal                      15.9
               Domestic Natural Gas              22.7
               Domestic Oil                      16.68
               Imported Oil                      18.91

Consumption]/ in key sectors  in 1977  was:

                                           Consumption (Quads/Yr.)
            Sector                          CoalN. GasOTl

    Electric Energy Generation            10.64       3.26     3.45
    Residential/Commercial                  .22        7.21      5.99
    Industrial                              3.14       8.65     7.60
    Transportation                          0.0          .54    20.0
                                     174

-------
A comparison on a percentage basis  between domestic reserves and con-
sumption  is given by Figure 1.

                               Figure  1

                   U.S. RESERVES VS. U.S.  CONSUMPTION
                              2% OIL 49%

                           2% NUCLEAR 3%
                              2% GAS 26%
                            94% COAL 18%

                               OTHER4%-
MEASURED U.S. RECOVERABLE            CONSUMPTION PATTERN
      ENERGY RESERVES

    TOTAL = 10,600 QUADS               TOTAL (1977) = 76.56 QUADS
Clearly,  it  can be seen that the Nation  needs a substantial  shift in
consumption  from oil and gas which are not abundant, to coal which is.
Because of the nature of the respective  markets, it would appear easier
to accomplish this shift initially from  the more centralized consumers
such as the  utilities and the major industrial plants.  The adminis-
tration has  set as a goal that the oil and gas consumption of this
sector be reduced fifty percent (50%)  of present consumption by 1990
and legislation has been enacted accordingly.

The interrelationship of our energy challenge with environmental goals
was previously noted.  In the near-term, we must burn more coal arid we
must burn it cleanly and economically, and this means we need additional
FGD options.  Key environmental  regulations affecting coal utilization
are outlined in Figure 2.

                               Figure 2

                       ENVIRONMENTAL  REGULATIONS
                       AFFECTING COAL UTILIZATION

       Clean Air Act - 1977
          o National Ambient Air Quality .'.Standards
          o New Source Performance Standards
                                  175

-------
           o  Prevention  of Significant  Deterioration Regulations
           o  Nonattianment Policy
           o  State Implementation  Plans
       Resource Conservation and Recovery  Act -  1976
       Toxic Substances and Control  Act  -  1976
       Clean Water Act -  1977
       Safe Drinking Water Act - 1974

Further, it is to be noted that the acid rain phenomena has been receiv-
ing considerable attention recently.   This interest could result in
new legislation and the need for retrofitting a  new breed of low cost FGD
systems into many existing coal  burning  installations if such sources are
proven to be major contributors to  the problem.

In summary, in terms of R&D objectives,  we need  the early supply of an
assortment of systems which enable  utilities  and major industrial  users
to operate reliably and economically on  coal  or  coal  derived fuels while
meeting all present and anticipated environmental  regulations.   Further,
it is important that some of these  systems be particulary oriented toward
retrofit applications.

ORIENTING THE DOE FGD ACTIVITY AND  PROGRAM

The Department of Energy, Fossil Energy  Assistant Secretary, pursues these
R&D goals with a broad based program of  which the Flue Gas Desulfurization
Program is a part.   The  DOE program is  basically a private sector assis-
tance program.  The Department seeks to  identify technologies with high
potential public benefit and seeks  to  promote their accelerated develop-
ment and demonstration by assuming  some  of the financial burden and risk.
The orientation of the FGD program  to  certain other FE programs can be
seen by Figure 3.

                                Figure 3

                   CLEANUP TECHNOLOGY CONTROL OPTIONS

-------
The Flue  Gas  Desulfurization  Program Is  operated from the Office  of Coal
Utilization's Division  of  Cleanup Technology  Development.  Other  programs
operated  from the  Division are  crosshatched in  the Figure.   Cleanup tech-
nology development is pursued through DOE  Field Technology  Centers  as
shown below by Figure 4.

                                Figure 4

                    CLEANUP  TECHNOLOGY  DEVELOPMENT

                          DEPARTMENT OF  ENERGFY
                  ASSISTANT SECRETARY FOR  FOSSIL ENERGY
                       OFFICE OF COAL UTILIZATION
               DIVISION  OF  CLEANUP  TECHNOLOGY  DEVELOPMENT
        I                    I                    I                       2
Morgantown Energy    Pittsburgh  Energy    Grand Forks Energy     Laramie Energy
Technology Center    Technology  Center    Technology  Center    Technology  Center
    (METO*             (PETC)                (GFETC)               (LETC)

*Lead Center

The Cleanup Technology  Division has sought,  since its creation in 1979,  to
build on the excellent  FGD  technology  foundation layed down by the private
sector and by EPA,  TVA  and  EPRI.   I am personally grateful  for the many
reports from them which have afforded  us the opportunity  to understand
and assess the technological choices.   Much  of our  initial  effort has
been in providing support to programs  initiated by  these  organizations,
and we intend to continue this  approach along with  our modest in-house
efforts, and to significantly expand our joint efforts with the private
sector.  The importance seen for this  program within DOE  is evidenced by
its growth from a modest $2.7M  in FY 1979 to a requested  $21.OM in FY
1981.  Our FY 1982  request  maintains the momentum of this rapidly growing
effort.  We believe we  will  contribute by bringing  the energy perspective
into FGD development.

DOE FGD R&D PROGRAM

Although the DOE FGD Program includes  some effort aimed at  improving the
reliability, operability and performance of  conventional  lime/limestone
scrubbers,  and includes some attention to new FGD approaches, the majority
of our effort is going  into what might be called the emerging or advanced
FGD systems.  This  affords  us the opportunity to select and pursue those
particular efforts  which would  appear  to offer the  mose benefits for the
markets which need  to be served in order that coal  utilization can be
maximized in the shortest time.

                                      ,177

-------
Figure  5  describes  those technologies which we  have tentatively chosen
to  evaluate and how and when these evaluations  might lead to large scale
utility and industrial  demonstration.

                                 Figure 5

                            EMERGING FGD SYSTEMS
    UTILITY DEMO (lOOmW)


    TECHNOLOGY
    EVALUATIONS

         DOWA

         DRY SCRUBBING

         AQUEOUS
         CARBONATE
         DUAL ALKALI

         MAGNESIUM
         OXIDE
         CHIYODA 121
    INDUSTRIAL DEMO
    PILOT READY
    TECHNOLOGIES (10mW)
    SUB-PILOT
    TECHNOLOGIES (ImWI
FY79

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Figure 6 identifies our  key  near-term needs and the candidates which we
are evaluating to meet these  needs.

                                 Figure 6

                     KEY NEAR-TERM  NEEDS/CANDIDATES
              Need

      Reliable, low cost, retrofitable FGD
      systems for eastern coal  applications
      which produce an easily disposable
      dry or gypsum waste product.
      Reliable, low cost FGD systems  for
      western coal applications with  low
      water consumption and manageable
      waste products
       Candidates

o  Forced Oxidation Systems
o  Systems  such  as:
   -  Chiyoda  121
   -  DOWA
o  Spray Dryers

o  Dry Injection
o  Spray Dryers
                                      178

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   o   Reliable, low cost regenerate  systems    o   PETC  technology  data  base  for:
      which  utilize coal for  reduction  or          -   Improved  steam  stripping
      regeneration                                 -   Direct  coal reduction
                                                  -   Improved  copper oxide/
                                                     gasifier  system

Detailed  discussions of these  needs and.the primary candidates which are
being evaluated are included  in  the paragraphs  which  follow.

EASTERN NEEDS

Foremost  on  our list of key needs  1s  the need to  provide  by  the early 1980's
reliable, low cost, retrofitable FGD  systems for  eastern  coal  applications,
which produce easily disposal  waste products such as  gypsum  or dry insolu-
able  solids  rather than sludge.  The  candidates for this  need  would  appear
to include the newer forced oxidation systems,  systems  such  as CHIYODA  121
and DOWA  and spray dryer systems.  We are particularly  encouraged  by the
recently  reported improved stoichiometrics for  spray  dryer processes which
show  them to have economic advantages even with higher  sulfur  coal.   Our
evaluation programs are as follows:

     0 EVALUATION OF FORCED  OXIDATION  SYSTEMS

       DOE  will study data from recent full-scale commercial  forced
       oxidation systems and  compare them with the projected  quali-
       ties of CHIYODA 121 and  DOWA.

     We expect to complete this  study in January  and  the  results
     might lead us to initiate an  evaluation effort.

     o EVALUATION OF GYPSUM  WASTE SYSTEMS

       - DOE has tentative  plans to join with EPRI  in evaluating a full
          size CHIYODA 121 module.

       - DOE may support additional DOWA efforts at the TVA  Shawnee
          Test Facility.

   We also  believe that much  can  be  learned by carefully studying the
   results  of the recently completed CHIYODA 121  pilot scale  (23 MWe)
   tests.

   0 EASTERN COAL SPRAY DRYER  EVALUATIONS

      -   Eastern Coal Spray Dryer development/evaluation at pilot
          scale (RFP - early  FY  1981  award)

      -   Spray Dryer evaluation at PETC 500 #/hr coal-fired boiler.

      -   Spray Dryer performance  characterization at ANL on 170,000
          #/hr steam boiler (Preliminary)


                                       179

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       -  Joint EPA/DOE/EPRI  Spray  Dryer  characterization at 100 MWe
          utility unit (Preliminary)

As noted previously,  the  optimistic projection  for the application of
spray dryers to eastern coals is  recent and,  accordingly, our program to
increase emphasis in  this area  is not  completely  in place.

Our primary approach  is to pursue this evaluation through the private
sector and, accordingly,  we have been  preparing an RFP for such an evalu-
ation.  This RFP, which is scheduled  for  release  in October, offers to
fund pilot scale testing  of eastern coal  optimized spray dryer on a slate
of eastern coals, and offers further  to fund  the  conceptual  design and
economic evaluation of commercial scale units.

Parallel with this effort, we propose  to  obtain parametric performance
data on a subpilot unit at our  Pittsburgh Energy  Technology  Center (PETC),
and to take advantage of  the installation of  a  spray dryer being installed
on a 170,000 Lb/Hr. steam boiler firing eastern coal  at the  Argonne National
Laboratory (ANL).

Further, it is to be  noted that DOE,  in conjunction with EPA and EPRI, have
been discussing Spray Dryer characterization  testing on a 100 MWe utility
unit and such a unit could be used  to  verify, at  a large scale, the per-
formance projections  derived from pilot scale evaluations.

WESTERN NEEDS

For western markets,  we see the need  for  reliable, low cost  systems, with
low water consumption and manageable waste products.   Key facets of our
western applications  program are  as follows:

     o  EVALUATION OF DRY SCRUBBERS FOR WESTERN APPLICATIONS (GFET.C)

        -  Field testing  of full-scale utility  Spray Dryers  with lime
           and sodium reactants.

        -  Continued  testing and  evaluation of  dry injection of alkaline
           ash, nahcolite and trona and the regeneration of  reactants.

REGENERATION WITH COAL

We see the need for reliable, low cost regenerable systems which can
utilize coal  for reduction or regeneration, and we are approaching this
need at this time with in-house laboratory tests  and studies.  This
program is as follows:

     o  PETC TECHNOLOGY BASE FOR  IMPROVED REGENERABLE FGD SYSTEMS

        -  Model  the  reaction dynamics for direct reduction  of S02
           with coal.  Verify at  bench scale.

        -  Measure $62 partial  pressures for prospective organic
           absorbants to  optimize  absorption/steam stripping systems.
                                    180

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        -  Evaluate  at PDU scale a fluid bed reactor copper  oxide
           system  employing coal gas  as  a reducing agent.

It is our desire to  produce a data base  from which the private sector
might create or optimize improved regnerable systems which use coal
instead of oil or  gas for reduction or regeneration.

POTENTIAL NEW CHALLENGES/OPPORTUNITIES

As noted previously,  the attention being given to existing pollution
problems such as acid rain could precipitate the development of a new
breed of low cost, retrofitable, less than NSPS capture systems to which
our present plans  are not addressed.  We are looking carefully at the
work being sponsored by EPA in this area, and we will be joining them in
the Limestone Injection Multistage Burner (LIMB) effort.  In addition,
we have been evaluating burners, such as the staged slagging combustors,
under other FE programs, which might  employ limestone injection and
which might lead to  workable systems  for such applications.

A related challenge  might come from the  proposed Powerplant  Fuels Conser-
vations Act of 1980  (S. 2470).  While the major thrust of this proposed
legislation is to  mandate the conversion from oil to coal of approximately
18,000 MWe of powerplants primarily along the eastern coast,  it also con-
tains a very important "offset" provision.  The offset provision seeks
to offset the approximate 110,000 tons/hr of S02 additional  emission
caused by the conversion to coal, by  funding the addition of advanced S09
removal systems to approximately 3,000 MWe of existing coal-fired units."
To DOE, this is both a challenge in terms of being able to make wise
choices as to appropriate systems by  late 1982, and an opportunity for
increased development and demonstration  at a large scale.  Our tentative
plan for implementing the offset provision is shown below in Figure 7.

                                 Figure 7

                               GENERAL PLAN
    Program Definition
    • Track Legislative Action
    • Characterize SO2 Dlstr.
    • Characterize Regions
    • Characterize Candidates
    • Develop Plan
   . Budget
    • Input To FY 82 +
    Procurement
    • Prepare PON
    • Establish SEB
    • Solicit/Eval/Salect
    • Negotiate Grants
    Design/Construction
    Monitor
    Test Program
    • Establish Test Prog.
    • Monitor Tests
    • Analyze Results
    • Disseminate Results
                      Resource
  Supt.
  Supt.
  Supt.
  Supt
OCU/Supt.


  OCU

  OCU
  OCU
OCU/Proc
HDQ Proc


METC/OCU


OCU/METC
METC/Supt.
METC/Supt
 OCU/RA/
  EPRI
                                               SCHEDULE
         FY80  FY81  FY82   FY83   FY 84   FY 85   FY86
                                        181

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SUMMARY

In summary, DOE looks forward to joining with the flue gas cleanup
community in pursuing jointly both  our energy and environmental  goals,
and to contribute to the overall  success through our perspective of
the nations energy needs.

We are pleased with the opportunity to share with you our plans  and our
thinking, and we look forward to  the opportunity to  get to know  all  of
the participants better, and to work together toward these important
national  goals.
                                   182

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       EPRI RESEARCH RESULTS IN FGD:  1979 - 1980


S. M. Dalton, C. E. Dene, R. G. Rhudy, and D. A. Stewart
            Electric Power Research Institute
                  3412 Hill view Avenue
              Palo Alto, California  94303
                        ABSTRACT

  EPRI has a research effort of approximately $10M/year in
  flue gas desulfurization covering engineering evaluations,
  field testing, bench testing, pilot plants, prototypes and
  demonstrations.  This paper reports selected results from
  projects on FGD water integration, gypsum crystallization,
  limestone dissolution, wet stack operation, sulfur produc-
  tion via RESOX, absorption/steam stripping, cyclic reheat,
  and integrated emission control.  A brief review of current
  demonstration plans and program emphasis is also included.
                            183

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                         EPRI RESEARCH RESULTS IN FGD
                                 1979 - 1980
EPRI'S WORK IN FGD
The Electric Power Research Institute (EPRI), as the research arm of the U.S.
electric utility industry,  has established a research and development program
in flue gas desulfurization.   In this area, the Institute will fund approxi-
mately ten million dollars  of R&D work each year over the next five years.
Projects include engineering  evaluations,  laboratory testing, pilot plant
work, prototype development,  demonstration installations and field testing.

CONTENTS OF THIS PAPER

In this paper are presented recent data from selected EPRI projects in the
areas of FGD field testing, economic evaluations, limestone dissolution, wet
stacks operation, FGD water integration, cyclic reheat, crystallization,
sulfur production via RESOX,  absorption/stream stripping, and integrated
emission control.  Also included in the paper is a discussion of EPRI's R&D
program emphasis in the next  few years.   Each project that has significant
recent results is discussed under a separate heading for that project.

OBJECTIVES OF THE PROGRAM

EPRI's FGD research efforts are designed to meet one or more of the following
objectives:

    Reduce costs:                   Reduce capital, operating, maintenance .and
                                    disposal costs.
    Improve reliability:             Identify reliable systems or components;
                                    develop improved materials; identify
                                    mechanisms and modes of failure, and
                                    repair requirements.
    Improve resource utilization:    Improve energy efficiency; reduce depen-
                                    dence  on oil, electricity and gas; reduce
                                    water  consumption and discharges; improve
                                    by-product utilization.
                                       184

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The specific  projects discussed in this paper represent recent EPRI funded
work not  reported separately at this symposium.   Papers are being presented in
other sessions covering successful testing of a 23 MU Chiyoda Thoroughbred 121
system with gypsum stacking at Gulf Power's plant Scholz, joint EPRI/TVA/UOP
testing of the 10 MW Dowa prototype, and EPRI solid waste disposal efforts.
These topics  will not be covered further in this paper*
                                        185

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      Projects discussed  in  this  paper:
Subject

Absorption
Steam
Stripping
Character-
ization of
FGD
Chemistry
 Corrosion
Crystalli-
zation

Cyclic
Reheat
Economics
EPRI Project
   Number

  RP1402-2
  RP1258-1
  -2,3,4
  RP1410-3
  IPS79-747
  RP982-21
  RP982-14
  RP982-19

  RP1031-2.3
                RP1652-1
  TPS78-760
  TPS78-767
               RP1180-9
Integrated     RP1646-1
Emission         1870-2
S0? Reduction  RP784-2
               RP1257-1

Water          TPS80-730
Integration
Wet Stack
Designs
  RP1653-1
Project Description

Lab and pilot development
of Flakt Boliden citrate
and novel steam stripping
processes

Test two FGD units compre-
hensively to establish
operating capabilities
and material and
energy balances.

Mg dissolution from
1imestone to improve
scrubber performance.

Lab testing of corrosion
and erosion in FGD.

Bench Scale sulfate
crystallization

Economic and field
evaluation of the cyclic
reheat concept (using inlet
heat to reheat)

High S02 removal
Design and Economics
Vol 1 Design
Vol. 2 Economics

Economic and Design Fac-
tors for FGD Technology

Build and test pilot
2-1/2 MW integrated
facility

RESOX pilot and prototype
development.

Material balance to show
effect of different water
sources on various FGD
systems

Entrainment and engineer-
ing for wet stacks
                                                      Contractors

                                                        U of Texas at Austin
                                                        (Dr.  Rochelle), TVA,
                                                        Steams-Roger, Radian
                                                        Black & Veatch,
                                                        MR I,  PEDCO,  TRW
                                                        Radian Corp.
                                                        Battelle Columbus
                                                        SumX  Corp.

                                                        U.  of Arizona
                                                        (Dr.  Randolph)

                                                        Bechtel  National Corp.
                                                        (Companion studies)
                                                        Radian Corp.
                                                        SRI  International
                                           Bechtel  National
                                                        Stearns-Roger,
                                                          et al
                                                        Foster Wheeler Energy
                                                        Corp., et al

                                                        Radian Corp.
                                          Dynatech   R/D  Co.
 EPRI
Contact

 D. A. Stewar
 R.  G.  Rhudy
 D.  A.  Stewar



 R.  G.  Rhudy
 C.  E.  Dene.

 D.  A.  Stewar


 R.  G.  Rnucy




 R.  G.  Rhudy




 C.  R.  McGowir
                                                                  D. V. Giovanni
                                                                   T. M. Morask)
                                                                   T. M. Moras*)
                                                                   D. A. Stewart
                                                                   R. Kosage
                                                                                C.  E.  Dene
                                             186

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RESULTS  SUMMARY  HIGHLIGHTS
Absorption/Steam  Stripping
Characterization
Chemistry
Corrosion
Laboratory work has confirmed the Flakt-Boliden
citrate process data, identified several poten-
tial stream stripping process improvements, and
set the stage for 1 MW pilot plant testing at
TVA's Colbert plant facility.

Two FGD units have been tested, the Col strip
Unit 2 of Montana Power Co. and the Conesville
Unit 5 of Columbus and Southern Ohio Electric
Co.  Some details of the test results are given
in the attached writeup.

Certain magnesium-containing limestones may be
more reactive than high-calcium stones depend-
ing on the minerology.  Three promising stones
have been identified for further screening.

Surveyed installations and manufacturers and
identified downstream ductwork, stacks, dampers
and expansion joints as special problem areas.

Evaluated chemical additives as corrosion
inhibitors and identified N-lauroylsarcosine
for further evaluation.
Crystallization
Developed calcium sulfate crystal growth pre-
dictive equations, evaluated certain crystal
habit modifiers, and found a crystal!izer con-
figurations which may help in controlling
gypsum crystal size.
                                       187

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Cyclic Reheat
Economics
S02 Reduction
Water Integration
 The  use  of  inlet  heat  to  reheat  exhaust gases
 appears  to  break  even  economically  with steam
 reheat for  moderate  steam costs  when using
 high-cost alloy for  the cyclic reheat  system.
 The  low  sulfur coal  full-scale cyclic  reheat
 system was  tested and  found to be working
 well.  High sulfur coal cyclic reheat  economics
 depend on construction material, degrees of
 reheat,  and inlet flue gas temperature.

 Several  special purpose evaluations  were per-
 formed.  Regenerable processes generally are
 more expensive for the specific cases
 studied.  High S02 removal design studies
 (TPS 78-760/1767) identified potential  for
 effect of Mg  in reducing  high S02 removal  costs
 in conventional FGD.  Generalized case  studies
 (RP1180-9)  identified  spray drying  as  a cost
 saving technique for western FGD and CT-121 as
 having low  lifetime  costs.  Under RP784-1, the
 possible benefits of absorption/steam  stripping
 combined with RESOX were  identified  (though
 these were  not verified in later work).

 Pilot work  at 1 MW scale  has verified  RESOX
 suitability for different types of coals and
 for different S02 feed stream concentrations.
 German 42 MW prototype efforts have  not shown
 high sulfur yields or sustained operating
 times.

 Over forty material   balance cases have  been
 evaluated.   Several  cases show increased
 scrubber scaling potential with certain sources
of water.
                                       188

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Wet Stack Design               Based on a literature search and theoretical
                               calculations a significant portion of the water
                               present in the stack appears due to carryover
                               from mist eliminators.   Design criteria from
                               existing wet stacks and the problems
                               encountered are identified in the attached
                               write-up.
                                        189

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                     ABSORPTION/STREAM STRIPPING  PROCESS
                             RP1258 and RP982-20
OBJECTIVE
Regenerate processes for S02 removal  from stack gases are being investigated
in order to hasten development of an economically feasible FGD process alter-
native to the throwaway systems.   Initial  cost comparisons of several pro-
cesses indicated that absorption/steam stripping may be an economically com-
petitive FGD process.

PROJECT DESCRIPTION

A project was initiated in 1978 to study the Flakt-Boliden absorption/steam
stripping process as it was the most technically advanced.  Laboratory con-
firmation of basic process and pilot plant construction were conducted conc-
urrently followed by pilot plant  tests to  obtain firm data for design and cost
studies.

RESULTS

In the absorption/steam stripping process, S02 is absorbed in a buffered
solution and then stripped from the solution with steam.  The stability of the
dissolved S02 in the buffered solution is  an important factor in S02 recov-
ery.  Loss of the dissolved S02 may result by disproportionate or by reac-
tion with another component, such as the buffer or oxygen.  The results of a
study of the stability of S02 in  the two most important absorbents, sodium
citrate and diethylenetriamine (DETA), are shown in Table 1, along with the
stripping steam requirement.
                                      190

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                    TABLE  1   Loss  of SOg from Buffer Solutions
                                                 Loss Rate
                                                x 103, M/hr
                                                    1.2
                                                    3.3
                                                    8.9
                                                   23»0
                                                    2.9
                                                    6.2
                                                   12.0



Buffer
Citrate



DETA




Buffer
Cone., M
0.5
0.5
0.5
0.75
2.0
2.0
2.0
Initial
dissolved
S0?
Concf M
0.2
0.2
0.2
0.2
0.08
0.2
0.2



Temp, °C
140
150
158
163
139
145
155
Estimated
Stripping
Steam Rate,
Kg/Kg S02
   40
   20
DETA solutions do  not  appear to retain SOp as easily as citrate solutions.
The savings  In steam costs are the primary reason for continued investigation
of DETA.   Comparisons  of  stability of the absorbents, citrate and DETA, are
being made.

FUTURE WORK

The pilot plant  study  of  the Flakt-Boliden process (citrate absorbent)  is
currently underway at  the Colbert Station of the Tennessee Valley Authority.
Following analysis of  the data from this test program, further pilot tests
will be conducted  with either citrate or DETA.  The extent of the test  program
with DETA depends  on the  results of the laboratory work on DETA stability.
                                       191

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                  CHARACTERIZATIONS OF  FULL-SCALE  SCRUBBERS
                                   RP1410-3
OBJECTIVE
The full-scale scrubber characterizations project was initiated  in order to
provide the needed data base to enable the utilities to optimize their exist-
ing systems effectively, to aid them in selecting new systems, and to provide
informed utility responses to possible new emission standards.

PROJECT DESCRIPTION

The project is directed at performing extensive and detailed characterizations
of the capabilities of selected, representative, currently operating, full-
scale lime and limestone wet scrubbing systems.  The program characterizes the
performance of the selected scrubber system with respect to the following:

    o    Meeting emission standards and performance guarantees, with emphasis
         on sulfur dioxide removal.
    o    Quality and quantity of selected unregulated discharges for such
         species as organic compounds, volatile metals, fine particulates, and
         trace elements.
    o    Actual costs compared to estimated costs, including both capital and
         operating costs.
    o    Reliability, availability, and operability.

The initial scrubber systems selected for characterization are Columbus and
Southern Ohio Electric Company's Conesville Unit 5 and Montana Power Company's
Colstrip Unit 2, burning high sulfur eastern coal and low sulfur western coal,
respectively.

RESULTS AND CONCLUSIONS

Work has been completed at Conesville and a draft final report is in review.
Field testing has been completed at Colstrip and the data are being analyzed
prior to preparation of a final  report.
                                      192

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Conesville Unit 5 is a 411 megawatt power plant which began operation  in
January,  1977.   The flue gas cleaning system for this unit consists  of a  cold-
side electrostatic precipitator followed by a turbulent contact  absorber
scrubbing system capable of greater than 90 percent sulfur dioxide removal
from a high sulfur coal.  Magnesium containing lime is used as the scrubber
additive  and the scrubber sludge is stabilized by a commercial "fixation"
process and stored onsite in a landfill operation.

With respect to regulated emissions, greater than 95 percent S02 removal  was
measured across one module of the two-module system.  Although the net S02
removal is decreased for Unit 5 because of a system bypass and these measure-
ments were short term (8 hours), the presence of a high level of dissolved
alkalinity provided by the magnesium in the lime would allow a reduction  of
one third in pumping power (3 pumps to 2 pumps) with only a 1 to 2 percent
change in the S0£ removal.

The particulate removal across the module measured was always positive.   The
particulate removals may not be representative because the inlet values were
higher than expected (suggesting either high inlet ESP loadings  or non-optimum
ESP operation)  and the outlet values may be affected by SOj condensation
across the scrubber.  However, no evidence was found to indicate a significant
scrubber related particulate emission increase.  Removal of NOX  was  insignif-
icant.

The condensation of 503 across the scrubber created problems in  the  particu-
late size distribution measurements.  The only particulate penetration
measured, in the 0.1 to 0.2 ym range, was attributed to sulfuric acid  conden-
sation based on the size, appearance, and elemental composition  of the mater-
ial captured.  The trace element data is still being reviewed and  it  is too
early to present the results.  The measurements of organic emissions  indicated
few were present and what was measured was well below its toxic  level.

Average availability of the Conesville Unit 5B scrubber module from  January
1979 through August 1979 was 39.2 percent.  If major outages which resulted
from labor problems, failure of major equipment components, and  design changes

                                      193

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are subtracted for this period, maximum expected availability would increase
to about 68 percent.

The remaining 32 percent of module unavailability is due to a variety of
maintenance requirements, such as  cleaning  plugged lines, cleaning scrubber
modules, and repairing equipment which had  malfunctioned.  A vigorous record
keeping plan has been initiated by the operating utility which will  allow
identification of individual  maintenance problems in the future.   Maintenance
levels on the unit have been  substantially  increased and the current availab-
ility of the unit is  close to the  boiler availability.
                                     194

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CHEMISTRY OF MAGNESIAN LIMESTONE DISSOLUTION
RP982-21 and TPS80-730
OBJECTIVE

The presence of dissolved magnesium In lime or limestone FGD systems generally
Improves the S02 absorption due to an associated increase in disolved
alkali.  However, the magnesium present naturally in limestone is usually in
the form of dolomite, which is too slowly soluble to significantly increase
the magnesium ion concentration.  Recently, a few limestones containing
greater than 1% MgCOj (magnesian limestone) have been tested which appear to
have a portion of the magnesium in soluble form.

To determine if magnesian limestones containing soluble magnesium compounds
are common, a survey of the literature was conducted to locate limestone
formations containing greater than 3% MgCOg but less than pure dolomite (46%
MgCOg).  These formations have been sampled for chemical and mineralogical
analyses and solubility and rate of dissolution determinations.

PROCEDURE

Samples of 12 different magnesian limestones have been taken directly from *ne
quarries.  These quarries are mostly in the east and midwest.  Samples of sane
western U.S. limestones are also available for study.  Characterization of the
stones includes chemical analyses for major constituents, X-Ray diffraction to
determine mineral content, and optical and electron microscopy to determine
grain size.  Selected stones were tested for equilibrium solubility in water
by mixing a ground sample with water, agitating at a constant temperature, and
analyzing with time to a constant composition.  The rate of dissolution of
ground limestone 1s determined by adding limestone to simulated FGD liquors
and analyzing with time.  The effects of limestone particle size, temperature,
rate of agitation, pH, and Initial solution composition on solution rate are
being studied.
                                      195

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RESULTS AND CONCLUSIONS

Ten magnesian limestone samples from different formations have  been  subjected
to X-Ray diffraction analysis.  Of these stones, three contain  portions of the
magnesium in a form other than dolomite.  A comparison of the rate of  dissolu-
tion if MgC03 from these three samples will be compared to rates of  a  dolomite
stone and calcite stone.  Preliminary results from a study of the effects of
variables such as particle size, temperature, rate of agitation, pH  and solu-
tion concentrations on the rate indicate that these variables affect the rate
of solution by different degrees for the different stones.  For example,
increasing temperature from 50°C to 60°C increases the rate of  solution of
CaC03 from Fredonia limestone but has little effect on rate from Maysville
Limestone (a magnesian limestone).

FUTURE WORK

The experimental  procedures described here will  be used on additional
limestone samples to determine if variables studied have any major effects on
rate of solution of either magnesium or calcium compounds in the limestone.
If the effects on solubility are not the same for each limestone, further
characterization of the limestone properties will be made in an attempt to
correlate limestone variables with differences in solubility behavior.
                                     196

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CORROSION INHIBITORS
RP982-17

OBJECTIVE

Corrosion complicated by erosion has been a continuing problem in wet scrub-
bing systems for flue gas desulfurization (FGD).  The attempts to solve these
problems  have been made using coatings, linings, and various metal alloys.
Despite these attempts, maintenance and replacement coats have remained very
high.

Techniques such as the use of corrosion inhibitors have not been seriously
investigated for corrosion prevention in FGD systems.  SumX Corporation has
undertaken a study for EPRI designed to determine the feasibility of using the
absorption type corrosion inhibitors in lime or limestone scrubbing solutions.

The major objective of this study is to determine if absorption inhibitors can
be used to lessen corrosion in FGD equipment.

PROJECT DESCRIPTION:

The work  consists of laboratory experiments using electrochemical techniques
to detect changes in the corrosion potential of the metal in scrubber liquors.

Data from literature as well as recommendations from inhibitor suppliers were
used to select inhibitors for preliminary screening.  The effect of these
inhibitors on the corrosion of mild steel, 304L stainless steel and 316L
stainless steel under one set of solution conditions was measured.

RESULTS AND CONCLUSIONS:

To date 10 compounds have been tested with mild steel.  N-Lauroylsarcosine has
shown the best inhibitor properties.  Sulfite concentrations appear to have a
major influence on corrosion.  The formation of a reaction film can be crit-
ical to the corrosion rate.
                                      197

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Tests conducted with stainless steels are incomplete; however,  uniform  cor-
rosion rates are very low.   The major influence on corrosion observed thus far
has been temperature.

Future work on this project will  involve compounds related to N-Lauroylsarco-
sine, completing tests with 304L and 316L stainless steels.  In addition,
tests to determine sensitivity to inhibitor concentration and other solution
characteristics will  be conducted.   Coupon tests with slurry solutions will be
performed for extended periods with the most promising inhibitor compounds.
                                     198

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CORROSION AND MATERIALS OF CONSTRUCTION
RP982-14

OBJECTIVE

The objective of the materials of construction in wet scrubbers project was to
comprehensively document and analyze the utility experience with materials of
construction in full-scale lime and limestone wet FGD systems on boilers
burning eastern or western coals.  The result will be a summary of materials
experience.

PROJECT DESCRIPTION

Information on field performance of construction materials was collected
primarily by site visits, but also by telephone and letter contacts with FGD
system operators and equipment vendors, and by literature searches.  Informa-
tion was collected for the following FGD system components:  prescrubbers,
absorbers, spray nozzles, mist eliminators, reheaters, fans, ducts, expansion
joints, dampers, stacks, storage silos, ball mills, slakers, pumps, piping
valves, tanks, thickeners, agitators, rakes, vacuum filters, centrifuges, and
pond linings.

Materials documentation and analysis include successes, failures, reasons for
success or failure, failure mechanisms, and relative costs of various mater-
ials.  Detailed trip reports on each site visit are included in an appendix.
The results are designed to be a first step in aiding utilities and FGD equip-
ment suppl iers in selecting materials that will perform satisfactorily at
minimum expense.

RESULTS AND CONCLUSIONS

Stack linings and outlet ducts (beyond outlet dampers) are the scrubber com-
ponents that have a significant history of materials problems and are critical
components in that failures may require complete boiler shutdown and loss of
generating capacity for lengthy periods due to the lack of standby components
or bypass capability.

                                      199

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The performance of a stack lining depends on whether the  scrubbed  gas  is
delivered to the stack wet or reheated, and whether or not the  stack is  also
used for hot bypassed gas.  These factors appear to have  a strong  effect on
the performance of lining materials, in spite of differences  in fuel sulfur,
application techniques (e.g., surface preparation or priming),  operating
procedures (e.g., thermal shock), design (e.g..annulus pressurization),  and
other factors which can  affect performance.

Inlet and bypass ducts are generally not a major problem  area for  utilities
with scrubbers.  However, the outlet duct has been a major problem area,
particularly for units which have duct sections which handle both  hot  and wet
gas.  These sections are for the most part beyond the bypass junction  on units
which do not have reheat.  Acidic conditions developed during scrubber opera-
tion become more severe on bypass as the temperature is raised  and other
corrosive species in the unscrubbed flue gas (chlorine and fluorine) are
introduced.

Research efforts for these two components need to be directed to:

    1.   Compiling and maintaining general  materials performance data
    2.   Characterizing environmental conditions where failures are occurring
    3.   Post-testing materials exposed to FGD environments to determine
         and/or verify failure mechanisms
    4.   Laboratory testing of commercial materials to verify proprietary
         data, and
    5.   Developing new or improved materials and designs based on the above
         information.

Prescrubbers, absorbers, reheaters, outlet ducts ahead of the outlet dampers,
dampers, pumps, and piping and valves have a moderate history of materials
problems but failures may not require complete boiler shutdown.  Spray noz-
zles, mist eliminators,  fans, inlet and bypass ducts, expansion joints,  stor-
age silos, ball mills, slakers, tanks, thickeners, agitators, rakes, vacuum
filters, centrifuges, and pond linings have a relatively low history of  mater-
ials problems and/or are amenable to rapid repair or replacement.
                                       200

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CRYSTALLIZATION OF  GYPSUM
RP1031-2

OBJECTIVE

Forced  oxidation  with gypsum crystallization is being proposed as a means of
solving or  reducing the  problems of handling sulfite sludge.  Production of
gypsum  offers  two alternatives to landfill sludge disposal.  One alternative
is to produce  a gypsum of sufficient purity and consistency to be used in the
manufacture of wall board.  The other is to produce gypsum of sufficient size
to result  in easy dewatering allowing "stacking" as another means of disposal.

In order  to design FGD systems which will consistently produce a product of
the desired properties,  basic crystallization data are necessary.  To obtain
these data, a  study of the nuclcation rate and growth rate of gypsum has been
completed.   In addition, the effects of some operating conditions and
additives  on these properties were determined.

EXPERIMENTAL PROCEDURE:

Determination  of  nucleation and growth rates of gypsum were made in the "mini-
nucleator"  developed at  the University of Arizona.  The crystal!izer in this
apparatus  is a one-liter, draft-tube-baffle, jacketed, glass vessel.
Provisions  are made to control temperature, liquor flow, and
supersaturation.   A particle counter by Particle Data, Inc. connected to a
PDP-8 mini-computer is used to count particles and analyze data.

Supersaturation  is normally developed by dissolving a desired compound at one
temperature and crystallizing at a lower temperature for systems where
solubility  is  temperature dependent.  However, CaS04 has a low solubility and
supersaturation was maintained by chemical reaction.  Liquors were both
simulated  and  actual limestone scrubbing liquors.  Process variables studied
were pH,  agitation rate, and seed crystal concentration.  The additives
studies were sodium dodecylbenzenesulfonate, Calgon® CL246, adipic acid, and
                                        201

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citric acid.  These data were used in a computer simulation program to  predict
gypsum crystal size distribution from various crystallizer designs.

RESULTS AND CONCLUSIONS

Qypsum nucleates by secondary nucleation mechanisms of the collision breeding
type when large (>150yu.m) parent crystals are retained in the crystal  magma.
High supersaturation and/or an absence of parent seed can result in bursts of
excessive primary nuclei which degenerate particle size.

Although pH does not appear explicitly in the nucleation/growth rate kinetics
expressions, the ratio of nucleation to growth shifts at low pH levels to
produce smaller crystals.  Regions of low pH (or sudden decrease in pH) in the
scrubber system would be expected to reduce particle size.

Of the additives studied (sodium dodecylbenzenesulfonate, polyacrylate, adipic
acid, citric acid), only citric acid had a beneficial effect on the size and
shape of the crystals grown.

Computer simulations utilizing the nucleation/growth rate kinetics expressions
developed in this study, together with assumed crystallizer configurations,
indicate that particle size could be nearly doubled using a double-drawoff,
classified removal  crystalizer configuration in which mixed underflow and
partially settled overflow streams are removed from the crystallization
tank.  Such operation could be achieved simply by installation of an internal
settling baffle.

PLANS FOR FUTURE WORK

Since only one liquor composition was used in these studies, the effects of
other ion concentrations (e.g., chloride and magnesium) in both lime and
limestone system liquors will  be studied.  These data and the predicted size
improvments are  to  be verified in a bench-scale crystallizer system.
                                        202

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.CYCLIC REHEAT
 RP1652-1

 OBJECTIVE

 A significant  power  plant  operating  cost  savings  is achievable if the cost  of
 steam or oil used to reheat  flue  gas downstream of  SOg wet  scrubbing can be
 reduced or eliminated.   One  method of accomplishing this goal  is by use of  a
 cyclic reheat  system which extracts  heat  from the flue gas  entering the
 scrubber and uses that  heat  to  reheat the stack gas.   This  study was performed
 to achieve a better  understanding of cyclic  reheat  and to fill  in information
 gaps regarding its application.   The specific objectives are:

    o    To publicize the  status  of  research work on  cyclic reheat.
    b    To characterize the only existing U.S. full-scale  cyclic reheat
         installation at Southwestern Public Service's (SPS) Harrington
         Station Unit 1 near Amarillo, Texas.
    o    To provide  an  economic comparison between  cyclic reheat and conven-
         tional  stack gas  reheat  schemes.

 PROJECT DESCRIPTION:

 The approach used to accomplish these objectives  and develop the study infor-
 mation can be  summarized as  follows:

     o     Information on cyclic  reheat research activities was obtained by
         literature  search and  by discussions with  users, vendors, and
         research and engineering institutions regarding equipment types and
         systems used or considered  for this application.
    o    Characterization  of Harrington Station's cyclic reheat system was
         conducted by collecting  historic design, cost, operating, and main-
         tenance data;  by  performing gas  sampling,  component analyses, and
         temperature and pressure measurements on selected  streams; and by
         analyzing these test data for system performance.
    o    Economic comparisons of  cyclic reheat and  three conventional stack
         gas reheat  systems  (in-line steam,  hot-air injection, and oil-fired

                                       203

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         reheat) were made on a comparable basis for both  low  and  high  sulfur
         coal cases.  The comparisons are based on two 500 MW  units  operating
         with a reheat level of 50°F and with inlet flue gas (after  dust
         collection) temperatures of 300°F and 270°F, respectively for  the
         high and low sulfur cases.  Materials of construction of  exchanger
         tubes are chosen to take into account the sulfuric acid dewpoint and
         the temperature level of the reheat medium.  Capital  and  operating
         costs are presented on a 30-year levelized basis.  Cost sensitivity
         analyses were performed to determine the effect of certain  design and
         energy value parameters.

RESULTS AND CONCLUSIONS

Results of the review of cyclic reheat research activities indicated that
considerable effort has been and is being conducted on different approaches
and  equipment types.  Most experience in the United S,tates has been with
gas/liquid/gas (Harrington) type systems, while in Japan it has been primarily
with regenerative gas/gas (Ljungstrom) type cyclic reheat.  Other  approaches
and  equipment types in use or being studied include:  (1)  a heat pipe concept
consisting of a closed tube containing a heat transfer medium  which  vaporizes
during heat extraction and is condensed in reheating the scrubber outlet gas,
(2)  a borosilicate glass tube exchanger for gas/gas'type cyclic reheat, and
(3)  a cast iron finned tube exchanger for low level heat recovery  in a
gas/liquid/gas system.

Characterization of cyclic reheat at Harrington Station which  uses low-sulfur
coal  (0.3 to 0.5% sulfur) indicated superior operating experience with  no
serious corrosion or plugging problems despite carbon steel construction of
the  heat extractor and reheat exchangers.  Results of the  field test program
indicated performance of the cyclic reheat and FGD systems are reasonably
close to design.   Sulfur trioxide (S03) content measured in the flue gas feed
to the heat extractor was found to be considerably less than expected and
indicates probable absorption and neutralization by the alkaline fly ash
either in the flue gas or in the sampling system.  Average finned  area  heat
transfer coefficients  for the heat extractor and reheat exchangers were found
experimentally to be 6.3 and 10.3, respectively, as compared with  values of
                                      204

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9 to 10 from  accepted correlations when assuming the same flow conditions and
a clean surface.

Results of screening-type capital estimates for both the Ljunstrom and heat
pipe schemes  indicated that these cyclic reheat approaches may have some cost
advantage over the gas/liquid/gas system.  However, a gas/liquid/gas system
similar to that operating at SPS1 Harrington Station and to that being
installed at TVA's Paradise Steam Plant was chosen as a base case for com-
parison with  conventional reheat methods because of the greater experience and
availability  of information.

Simplified EPRI Class 1 (±20%) capital and operating cost estimates were made
for the gas/liquid/gas type cyclic reheat system and for the three conven-
tional reheat systems, each with both high and low sulfur coal.  Results are
summarized in Table 2.
                TABLE  2   REHEAT  SYSTEM  CAPITAL  AND OPERATING COST SUMMARY
                       Basis:  2x500 MW coal-fired plant, Midwest
                               location, 30-year plant life, pricing
                               level-EOY 1979
                               HS - High-sulfur coal, 4.0% avg.
                               LS - Low-sulfur coal, 0.48% avg.
                               Capacity factor 70%
                                            In-Line        Hot-Air     Oil-Fire:
                          Cyclic Reheat   Steam Reheat   In. Reheat     Reneat.
                            HS
LS     HS
                         LS
HS    LS
HS    LS
Process Capital, $/kW     17.7     22.8    6.2     6.8    3.1   3.2   2.2
Total Capital, $/kW
First Year O&M Cost,
  $/kW
Level 1 zed Capital
Charges, milIs/kWH
Level1 zed O&M Cost,
mills/kWH
Total 30-year Levelized
Cost, mills/kWh
23.2     29.4    8.8     9.6    4.9   5.1   3.7
 1.9

 0.68

 0.60
2.2    4.1     4.4    9.5  10.6   5.0
                    2.4
                    4.0

                    5.5
0.86   0.26    0.28   0.14  0.15  0.11    0.12

0.69   1.30    1.42   3.04  3.40  1.97    2.17
 1.28     1.55   1.56    1.70   3.18  3.55  2.08    2.29
             205

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At the energy values of $2.90 per 1000 pounds ($6.39 per 1000 kg) for
70-250 psia (483-1724 kPa)  steam, $4.45 per 1000 pounds ($9.80 per 1000 kg)
for 250-600 psia (1724-4137 kPa)  steam, $4.40 per million Btu ($4.17 per GO)
for oil, and 31 mills per kWh for electric power assumed in this study, cyclic
reheat is estimated to have the lowest 30-year levelized total cost for stack
gas reheat.  Cyclic reheat  has the highest capital  requirement; direct
combustion reheat has the lowest.

Study conclusions and recommendations include the following:

    o    Considerable research activities on cyclic reheat are being conducted
         with promising results.   For low-sulfur coal  application, operating
         experience has been good at the Harrington Station of Southwest
         Public Service.  No serious corrosion or plugging problems are
         reported.  For medium-sulfur coal application (1-2% sulfur) satis-
         factory operating  experience is reported in Japan using the regenera-
         tive type of heat  exchanger (Ljungstrom type).  For high-sulfur coal
         application there  is currently no operating experience; however,
         TVA's Paradise Steam Plant FGD system using cyclic reheat with high-
         sulfur coal is expected  to start operation in 1982.

    o    The major advantage of cyclic reheat is energy savings.  This is
         realized at the expense  of higher capital  cost.  A simplified (EPRI
         Class I) estimate  indicates that when medium-pressure steam costs
         $2.30 per 1,000 pounds ($5.10 per 1000 kg) or more, cyclic reheat has
         an economic advantage over conventional in-line steam reheat for
         high-sulfur coal.  The breakeven point for low-sulfur coal application
         (based on an inlet flue  gas temperature of 270°F (132°C) instead of
         300°F (149°C)) is  $2.60  per 1,000 pounds ($5.73 per 1000 kg).

    o    The capital cost of cyclic reheat is quite sensitive to the inlet
         flue gas temperature,  which influences heat extractor size and mater-
         ials of construction.  Higher flue gas temperatures mean lower capi-
         tal  cost, but  penalize power plant thermal  efficiency.  The compara-
         tive economics of  a cyclic reheat system are also sensitive to the
         energy cost.   Therefore, each plant should be independently
         evaluated.
                                       206

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Cyclic reheat eliminates steam (or other fuels) consumption.  How-
ever, this energy saving is partially offset by additional gas-side
pressure drop across the exchanger surface.  The exchanger size is
influenced by the allowable pVessure drop.  High pressure drop
improves heat transfer and reduces exchanger size, but consumes
electrical energy in fan horsepower.  Pressure drop and heat
exchanger size must therefore be properly balanced to arrive at an
economic optimum.  In a gas/liquid/gas system, the design liquid
temperatures must also be chosen to minimize the exchanger cost
overall (extractors and reheaters).

Cyclic reheat reduces scrubber inlet gas temperature.  This has two
effects on the main FGD system:  (a) lowering the adiabatic satura-
tion temperature of the gas, and (b) reducing the process water
makeup requirement.  Lowering the adiabatic saturation temperature
may improve SOg removal efficiency, depending upon the particular FGD
system.  For the advanced concept of citrate absorption/steam strip-
ping, a lower operating temperature means reduced steam consumption
for S0£ stripping (Ibs steam/lbs $02).  Reduced process water makeup
may be beneficial in some arid areas; however, it also reduces the
water available for mist eliminator wash.  Both these factors are
significant in FGD system design.  Less water content in the scrubbed
gas may enhance visibility by reducing the vapor plume.

The rapidly escalating cost of energy has made cyclic reheat an
increasingly attractive alternate to conventional reheat methods for
FGD systems using wet scrubbing.  However, before large-scale adop-
tion of this reheat scheme takes place, several areas of uncertainty
such as corrosion, plugging, and cleaning of the heat extractor
should be investigated to minimize design errors and optimize equip-
ment cost.
                              207

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Future studies should include in-depth studies of the Ljunstrom-type
heat exchanger and of the heat  pipe for cyclic reheat application.
This would involve close monitoring of operating Ljunstrom-type
systems in Japan.
                            208

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ECONOMICS  OF  HIGH  SOg REMOVAL DESIGNS
TPS 78-760, 78-767

OBJECTIVES

This project  is a  team effort by Radian Corporation and SRI International. The
objective  of  Radian's work was to define representative cases and develop
process designs and material  balances that could be used to determine costs
for each case.   The process designs were developed using a process simulation
computer program developed by the contractor.  Cases were selected to span:

    o   Coal--eastern and western
    o   S02  removal— 84%, 93% and 99%
    0   Alkali—magnesia, limestone and lime
The objective of SRI's work was to use the results of the Radian work to
develop a  cost estimate for each case and then analyze the results.  The
latest vendor cost information was used to prepare the economic estimates.

PROJECT DESCRIPTION

This project  is composed of two separate technical planning studies that were
undertaken to predict the effect of potential increasingly strict S02 emission
limits on  the economics of wet scrubbing.  In the first study, Radian
Corporation performed process designs and material balances as input to the
second half of the study, an economic evaluation performed by SRI
International.

RESULTS

    Process Designs.  The major variables that were investigated in these
designs were  the liquid-to-gas ratio (L/G) in the scrubber and the volume of
the process slurry holding tank.  The former affects the S0£ removal effi-
ciency and the latter affects the scaling potential in the scrubber.
                                        209

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Under the study assumptions, higher S02 removals required moderate  increases
in L/G and were found to be dependent on the magnesium and chloride levels in
the slurry liquors.  This information is useful in gaining an understanding of
the magnitude of the process changes required for high S02 removals.

    Cost Estimates.  The study results are presented in Table 3.  For low-
sulfur coal systems, the design coal chosen meets the 1971 New Source
Performance Standard (NSPS) for S02 without any further S02 removal.
Increasing the design S02 removals to 93% and 99% results in a levelized cost
of 8.5 and 8.9 mills/kWh, respectively.  Magnesia scrubbing was about 7-8%
more expensive than limestone scrubbing on a levelized basis for the low-
sulfur western coal cases.  For eastern higher-sulfur coal, increasing the
removal requirements to 93% and 99% removal increases the levelized revenue
requirement by 8% and 18%, respectively.  Costs are significantly affected by
chloride and magnesium levels in the coal.  For high-sulfur coal, magnesia
scrubbing is about 15% cheaper than limestone scrubbing on a levelized revenue
basis.

The significance of the results of this study lies in the comparative numbers
and not in their absolute magnitude.  The increased costs are significant for
higher S02 removals but they do not change by an order-of-magnitude as origin-
ally anticipated.

Probably the most significant unanticipated result of the study was the large
effect that the Mg and Cl  content of the scrubbing liquor has on system design
and costs for lime and limestone systems.  It is clear that this area should
receive more attention in system design.

Finally, although the magnesia system appears less expensive than conventional
lime and limestone systems for high-sulfur coals, it is still not well
developed and its reliability remains uncertain.

Generalized cost estimates such as these are only an aid in planning either a
research program or the selection of a flue gas desulfurization (FGD)
process.   It is not appropriate to generalize these comparisons or assume they
represent manufacturers'  current selling prices.
                                        210

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                         TABLE 3    ECONOMIC  STUDY RESULTS
     System
Limestone
Limestone4
Limestone
Limestone (High  Cl)
Limestone (Low Mg)
Limestone (High  Mg)
Lime
Limestone
Limestone
Magnesia1*
Magnesia
Magnesia
Magnesia
Limestone
Percent S02
  Removal

    84
    93
    99
    93
    93
    93
    93
    93
    99
    93
    99
    93
    99
    93
  Type
of Coal1

 Eastern
 Eastern
 Eastern
 Eastern
 Eastern
 Ea stern
 Eastern
 We stern
 Western
 Eastern
 Eastern
 Western
 Western
 Eastern
   Leveli zed
    Revenue
 Requirement of
FGD. MilTs/kWh2

      13.0
      14.1
      15.4
      14.6
      13.8
      12.9
      14.1
       8.5
       8.9
      12.1
      13.1
       9.1
       9.6
      14.4
Total Capital
 Requirement,
    $/kW

     165
     194
     213
     204
     189
     178
     178
     123
     128
     193
     207
     155
     163
     181
1.  Eastern  coal,  4.0 sulfur; western coal, 0.48% sulfur; uncontrolled  emissions
    would be 7.5 and 1.1 Ib/million Btu, respectively.  Eastern  coal 0.1% Cl  in base
    case, 0.3% in  High Cl  case.

2.  Assuming an inflation rate of 6.0% per year and a fuel  cost increase of  6.2%  per
    year; 30-year  levelized revenue requirement at 1 eve!1 zed capacity factor of
    0.7.   Methodology standardized by EPRI.

3.  Base  cases.

4.  Variation of base case design.
                                        211

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ECONOMICS OF FGD
RP1180-9

OBJECTIVES

The overall objective of this project was to prepare a general and consistent
review of FGD technology economics.   Specific objectives were to:  (1) review
reasons for variations between published FGD cost estimates, (2) recommend a
consistent methodology for estimating FGD costs, and (3) prepare design and
cost estimates for alternative FGD technologies using this methodology.

PROJECT DESCRIPTION:

An economic evaluation of flue gas desulfurization (FGD) processes was
prepared by Bechtel National, Inc.  The report presents a review of published
FGD cost estimates, a discussion of the reasons for variations between
published FGD costs, a recommendation of a methodology for improving the
consistency of FGD cost estimates, and conceptual design and cost estimates
for eight regenerable and nonregenerable FGD technologies, based on the
recommended methodology.

FGD cost and performance estimates are presented for a new 2 x 500 megawatt
unit plant located near Kenosha, Wisconsin and fired by either a 4-percent
sulfur Illinois coal or a 0.48 percent sulfur Wyoming coal.  Other major
assumptions include 85 percent sulfur dioxide (S02) removal, four 33-1/3
percent scrubber modules, and redundancy in critical equipment.  The evalua-
tion was completed before promulgation of the final revised new-source per-
formance standards for S02 in June 1979.  Thus, the 70 to 90 percent S02
removal requirement was not used.

The FGD costs and other data presented in this report have also been used  in a
chapter on FGD economics in a report on sulfur oxides control technology being
prepared by the National Research Council's Commission on Sociotechnical
Systems.
                                      212

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EPRI intends  to update and report FGD cost estimates on a regular basis, as
technologies  change.

RESULTS

A review of nine published FGD cost estimates exhibited wide variations in
both estimated and actual  FGD costs.  These variations often reach factors of
three to five times the costs at the lower end of the cost range.  The major
causes of the cost variations are differences in S02 emission standard; scope
of estimate;  equipment redundancy; degree of design conservatism; purpose and
level of detail of estimate; and design and economic assumptions, including
coal type, plant location and capacity, and year of estimate.

The standard design and economic assumptions and methodology suggested in the
report are expected to reduce the magnitudes of the differences between esti-
mates.  This methodology is already being used in other EPRI-sponsored FGD
evaluations.

Conceptual designs and cost estimates are presented for the limestone slurry,
lime slurry, double alkali, Chiyoda Thoroughbred 121, Wellman-Lord magnesia
slurry, absorption/steam stripping/RESOX, and the lime slurry/spray
drier/fabric filter processes.

For both low and high sulfur coal applications, the alkali-based non-regener-
able processes exhibited the lowest capital and levelized revenue requirements
and the lowest parasitic energy consumptions.  The Chiyoda Thoroughbred 121
process appears particularly attractive.  It exhibits low total capital and
level ized revenue requirements and also produces a stackable gypsum byproduct
in lower volumes than the sulfite sludge byproducts produced by the other
limestone and lime slurry processes.  The spray drier/fabric filter process
using a lime slurry is also attractive, but has not yet been demonstrated for
high sulfur coal applications.  These costs are represented in the Figures 1
42.

The economics of absorption/steam stripping and other regenerate processes
are adversely affected by high energy consumption, principally for
                                      213

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ro
   -
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   LU
        200 i—
       150
    .
   «
   D.
   O
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   in
   O
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   «   100
   Q.
   to
        50
                HS
          LS
                       Process capital
                       General facilities
                       engineering and
                       contingency
                       Owner's cost
                    I
HS

LS
             I
HS
              1
LS

HS

LS
HS
                                                                            vvv
                                                                            LS
                                                                            HS
                                                            LS
                                                                                                            R&D
                                                                                                          Successful



                                                                  HS
                                                                                                        LS

                                                               HSl

                                                                                                    LS
                                                                                                                         HS
                                                                                                                   LS

 Basis:
              Limestone
                Slurry
                     Lime
                    Slurry
              Double
              Alkali
                       Chiyoda
                       CT-121
                          Wellman-
                             Lord
                                     Magnesia
                                      Slurry
New 2 X 500 MW coal fired plant, midwest location,
30 year plant life
Mid 1980 plant startup
  High sulfur coal - 4.0% sulfur (avg)
  Low sulfur coal - 0.48% sulfur (avg)
Capacity factor 70%, 6132 hrs/yr
85% SO2 removal
                                           Absorption/
                                             Steam
                                           Stripping/
                                             Resox  .
                                                        Spray Dryer/
                                                        Fabric Filter
                                                                                                            HS = High sulfur coal
                                                                                                            LS = Low sulfur coal

-------
    I
     0)

     e
    '3
     CT
     0)
    cc
     0)
cc
o
ro
M
01
    0>
    o>
  Basis:
         20
         15
     10
iL     5
                 HS
                 LS
                Limestone
                 Slurry
 Plant investment
 Owner's cost

   Total
   Captial
Requirements
     :LS
                                                    Fixed O&M cost
                                                    Variable O&M cost
                                            •
                                           •

                                                      HS
LS
                                           1
HS
                                              I
                                                                                                        R&D
                                                                                                     Successful
                                                                                                                       HS:
                                                                                                                      "LS:
                            Lime
                           Slurry
               Double
                Alkali
                                                     Chiyoda
                                                     CT-121
         Wellman-
           Lord
            Magnesia
              Slurry
       New 2 X 500 MW coal fired plant, midwest location,
       30 year plant life, 1979-2008
       Mid 1980 plant startup
         High sulfur coal - 4.0% sulfur (avg)
         Low sulfur coal - 0.48% sulfur (avg)
       Capacity factor 70%, 6132 hrs/yr
       85% SO2 removal
Absorption/
  Steam
 Stripping/
  Resox
Spray Dryer/
Fabric Filter
                                                                                                             HS = High sulfur coal
                                                                                                             LS = Low sulfur coal
                                        Figure  2     30 Year levelized FGD revenue requirements, 1979-2008.

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regeneration of the scrubbing reagent.  Under RP1258, EPRI is evaluating
improvements in the absorption/steam stripping/RESOX process that could reduce
both energy consumption and equipment costs.

Generalized cost estimates such as those presented in this report should be
used only as comparative estimates for research and development planning and
FGD process screening.   Since the estimates are based on a specific set of
assumptions, it is not  appropriate to generalize these estimates or assume
they represent manufacturers'  current, site-specific selling prices.
                                     216

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INTEGRATED EMISSION CONTROL PILOT PLANT
RP1646-1
RP1870-2

OBJECTIVE

The objective of EPRI's Integrated Emission Control (IEC) pilot plant research
effort is to provide utilities with engineering guidelines for the specifica-
tion of cost effective, reliable integrated emission control systems for coal
fired plants.

PROJECT DESCRIPTION:

An integrated series of 2-1/2 MW pilot plant modules have been or are being
constructed at EPRI's Arapahoe test facility in Denver, Colorado.  The facil-
ity extracts flue gas from Public Service Company of Colorado coal fired
unit.  The catalytic NO  control module and airheater are currently being
                       A
tested. Additional modules to be tested include a spray dryer, a wet scrubbing
system, a cooling tower, fabric filter and an electrostatic precipitator.  The
following elements or testing are planned:

    o    Complete characterization of each module and of integration effects.
    o    Implement a plant water chemistry program  including integrating the
         water loop.
    o    Investigate impact of flue gas temperature.
    o    Determine effect of ammonia on air preheater, scrubber and fabric
         filters (baghouses).
    o    Test baghouse and ESPs as a final collection device.

RESULTS AND CONCLUSIONS:

The catalytic NOX reactor has been operating since  March 1980 with NOX reduc-
tion performance close to original  design.  The test program is not far enough
along to allow for detailed evaluation.  Mr. Dan Giovanni, Program Manager of
EPRI's Air Quality Control Program, can answer any  general question on per-
formance to date.  The performance specifications for spray drying and wet
                                      217

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scrubbing modules have been released for bids.  A test sequence has been
defined for several  equipment configurations.  All these activities amount to
a multi-year R&D program that will  represent the first attempt to integrate
all of the best available control  technologies into a single facility.
                                     218

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SULFUR  PRODUCTION BY RESOX
RP784-2
RP1257-1

OBJECTIVE

The objective of EPRI's S02 reduction development efforts is to develop a
regenerable FGD process that produces elemental sulfur without using a reduc-
ing gas such as methane (natural gas) or producer gas (CO,H2).  The RESOX
process originally developed by Foster Wheeler Energy Corp. takes concentrated
S02 produced by various FGD absorption systems and converts it to elemental
sulfur by  reaction with hot crushed coal.

PROJECT DESCRIPTION

Several related projects have contributed to the EPRI sponsored development of
the RESOX technology.  Early cost estimates developed for EPRI pointed to
RESOX as a promising regeneration technique.  The development effort is two
fold with  a U.S. 1 MW laboratory effort in Livingston, New Jersey, and a 42 MW
demonstration effort in Lunen, Federal Republic of Germany.  Initial German
results were presented in a paper given in April 1979 at the ACS meeting in
Honolulu.

RESULTS AND CONCLUSIONS:

Initial sulfur production was in July, 1978.  Major equipment problems caused
extended outages and little run time from August to March 1979.  A total run
time of approximately 900 hours was obtained, with the most productive runs in
May and June of 1979.  Low yields of 65-74% elemental sulfur based on a sulfur
material  balance caused EPRI to postpone further German efforts until problems
were resolved in the lab.  Lab runs were undertaken in October-November, 1979
attempting to reproduce German conditions and to find an improved method to
correct the problem.  Both goals were met in the lab program and the problem
was diagnosed as overconversion of S02 to H2S and COS.  This was caused by an
imbalance  in gas flows, coal flow, and coal reactivity that led to high
temperatures and, thus, low sulfur yields.  The success of the improvement is
                                       219

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causing EPRI to seek patent protection for the invention.  Yields of  70% were
recorded when reproducing Lunen conditions, and yields of 82.1, and 83.8$ were
recorded using the improved method of RESOX operation.

In order to increase the applicability of RESOX, additional  lab work has been
done to ascertain that bituminous or subbituminous coals as well as anthracite
can be used as a reductant.  Testing using these types of coals was performed
with gases simulating Bergbau Forchung, Wellman-Lord, and magnesia off gas
(Chemico-Basic).  This testing was done without the improvement mentioned
earlier, which leads us to believe that yields and sulfur purity can be
increased.  Even without the improvement, it still  appears noncaking
subbituminous and bituminous coals can be used in the RESOX process and that
relatively dilute rich gas streams, such as magnesia off gas, can be
processed.  Coal types tested and results from this earlier testing are
summarized in Table 4 & 5.

                          TABLE 4    RESOX TEST COALS
      Mine/Seam

      Black Mesa/Yellow

      Seneca/Wadge
      Sophia Jacoba
 County/State

Navajo, Arizona
 Bituminous
Routt, Colorado
Ruhr, Germany
ASTM Ranking

High Vol C

Subbituminous A
Anthracite
                                      220

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                                      TABLE 5  RESOX TEST RESULTS FOR VARIOUS
                                                 COALS  AND FRONT-END  PROCESSES
                                      H20/S02
                                     Mol Ratio
                                                       S02 In
                                                     Feed (Mol %)
  Inlet S02
Conversion (%)
  El oriental
Sulfur Yield (%)
INJ
Bergau-Forschung Process
    Sophia Jacoba coal
    Black Mesa coal
    Seneca coal

Wellman Lord Process
    Sophia Jacoba coal
    Black Mesa coal
    Seneca coal

Chemlco-Basic Process
    Sophia Jacoba coal
    Black Mesa coal
    Seneca coal
2.2
2.2
2.2
2.5
5.0
6.0
5.0
5.0
4.0
20.7
12.0
15.3
24.4
14.0
11.8
8.3
8.3
9.0
90.0
92.1
86.4
91.3
88.7
84.5
91.6
88.3
82.6
79.5
85.2
71.8
80.0
82.7
75.0
79.7
69.4
68.1

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WATER INTEGRATION SIMULATION FOR LIME AND LIMESTONE FGD  SYSTEMS
TPS80-730

OBJECTIVE

Efficient utilization of water in power plants has become  increasingly
important particularly where water is scarce.  For those plants  which operate
a wet scrubbing flue gas desulfurization (FGD) system, minimizing water usage
requires careful study of overall water requirements with  possible  integration
of water treatment and disposal  in power plant and FGD systems.  It  may be
possible, for example, to use some power plant waste streams  in  an  FGD
systems.

PROJECT DESCRIPTION

To determine the effects of various water streams on the operation  of the FGD
system, a computer model which calculates stream compositions  for lime or
limestone wet scrubbing has been used.  This model will  accept two  different
water compositions per material balance calculation.  Approximately  40 differ-
ent cases using raw water and waste streams such as cooling tower blowdown,
and water treatment wastes in various combinations in the  FGD  systems have
been done.

Four different raw water sources ranging in total dissolved solids  (TDS) from
60 to 3400 ppm were chosen for study.  Other variables are coal  supply (one
eastern and one western), FGD system  (lime and limestone), prescrubber (with
and without), and S02 removal  efficiency.

These data were used in the Inorganic Process Simulator  program  of  Radian
Corp. to obtain reference material balances assuming that  raw  water  was the
only source of water for the FGD systems.  Various plant streams (cooling
tower blowdown, lime softening waste streams, etc.) were also  calculated using
these raw water sources in a computer program simulating cooling tower
operations.
                                       222

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To determine  if  an  FGD  system could utilize any of the cooling tower waste
streams  as makeup water,  combinations of raw water, cooling tower blowdown,
and treatment wastes  were used in the Inorganic Process Simulator was water
sources.  Material  balances,  scaling potential, operating conditions, scaling
potential, operating  conditions for the desired S02 removal, and stream com-
positions are determined  by this computation program.  Feasibility of using
the cooling tower  waste streams was judged by comparing the simulator waste
stream data to those  of the reference raw water data.

RESULTS AND CONCLUSIONS

Preliminary  results of simulations using an eastern coal are shown in Table 6,

TABLE 6    Simulation of Desulfurization of Eastern Coal Flue Gas
                    S02 in Flue Gas            3000 ppm
                    S02 Removal Efficiency     90%
                    FGD Absorbent              Limestone
  Makeup
Water Source
Lake Sakajawea
Santee River
Mississippi River
Cooling Tower Blowdown
  (Miss. River)

TDS
of Water, ppm


3470
66
458
8460


L/G Requi
gal/kft3
, i
96
129
129
86


red
(1/m3)

(12.8)
(17.2)
(17.2)
(11-5)
CaS03
Relative
Saturation


2.5
1.4
1.5
2.8
Simulations using a western low-sulfur coal  are  given  in  Table 7.
                                        223

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TABLE 7     Simulation of Desulfurlzation of Western Coal Flue Gas
                     S02 in Flue Gas
                     S02 Removal Efficiency
                     FGD Absorbent
  Makeup
Water Source
Lake Sakajawea
Mississippi River
Cooling Tower (Miss.
  River)
Cooling Tower
  (miss. River)
Cooling Tower
  (Lake Sakajawea)
     TDS
of Water, ppm
                           400 ppm
                           70%
                           Limestone
L/G Required
Absorber Effluent
 CaS03 Relative
   Saturation

3470
458
1530
8480
10,700
gal/kft3
15
62
53
25
9
0/m3)
(2.0)
(8.3)
(7.1)
(3.3)
(1.2)

0.7
0.1
0.5
1.8
1.5
The preliminary results show that the quality of the water used can affect
major variables such as L/G.  Effects of water quality on lime slaking, lime
and limestone availability and utilization, scaling, crystallization and mist
elimination can also be indicated by these studies and wil be included in
evaluations of the data as the work continues.
FUTURE PLANS

The simulator studies are to be continued using various combinations of water
and waste water streams.  Other coal, lime, and limestone compositions are to
be combined in the system calculations.  Build-up of impurities  (such as
chloride, sodium, and magnesium) will be calculated.  Laboratory tests will
then be completed to determine the effects, if any, on phase relationships,
crystallization of calcium sulfite and sulfate, reagent utilization, and
corrosion potential.
                                       224

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ENTRAINMENT IN WET STACKS
RP1653-1
OBJECTIVES

The history of wet  stacks  in the utility industry indicates two major problems
relative to their operation:   increased materials corrosion and mist genera-
tion.   This project' has  been directed toward the problem of mist generation.

PROJECT DESCRIPTION

The work involves the collection and evaluation of historical  data and
laboratory pilot research  on aerosol  emission (reentrainment)  from stack
walls.  The latter  work  involves experimental measurement of the critical
velocity where water droplets are removed from the condensate  film for the six
different combinations of  stack liner materials and construction roughness
shown below.

       STACK LINER MATERIALS  TESTED FOR  ENTRAINMENT  FROM  CONDENSATE  FILM

    1.   Acid resistant  brick (Custodis)
                                                       o
          Radical  tolerance of construction (3.3 x 10"Jm or 0.13 in)

    2.   Acid resistant  brick (Custodis)
          Radical  tolerance of construction 0.0

    3.   SI units CXL -  2000 coating
          Col bran  division of Pullman Power Products

    4.   Plastic coating No.  4005
          Vinyl Ester,  Wisconsin Protective Coating Corp.

    5.   Inconel alloy welded

    6.   FRP (Fiberglass reinforced  plastic) Alcore division of Custodis
                                         225

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 Included 1n the study is an evaluation of choke design  and  operation on a wet
 stack.  (The choke in a stack is the narrowing of the stack  diameter at the
 top or exit to increase velocity and aid in plume dispersion.)   This work
 includes experimental evaluation of two choke systems designed  with  water-film
 collectors.  Separation and reentrainment prevention techniques for  wet
 systems are also being evaluated using a mathematical model.

 Based on the operating experience, mathematical modeling  and  experimental
 work, a set of guidelines for acceptable wet stack system designs will  be
 formulated.  The guidelines documents will include criteria  for the  selection
 of duct size and stack diameter, and a discussion for the trade-off  between
 liner construction and critical reentrainment velocity, and  the need for
 reentrainment prevention techniques or entrainment separation devices.   The
 information is intended for use by A&E firms and utility  owners to select or
 review wet stack system designs.

 RESULTS AND CONCLUSIONS:

 Tables fi and Pwinddcate-'swneoof t^eeinfornra-tiow^thatthJ^Lbeen-iodat&iTffitlJih-i the
 survey of wet stack operating experience.  Based on literature  and laboratory
 measurements a properly operating mist eliminator carryover  rate is
 0.23-2.3 g/m3 (0.1-1 gr/ft3).  Under upset conditions this can  reach as  high
          o         O
 as 9.2 g/nr (4 gr/ft°).  Theoretical estimates of stack condensation range
 from 0.11-0.55 g/m3 (0.05-0.24 gr/ft3).  If the measurements and estimates are
 accurate, the mist eliminator carryover is a significant  portion of  the
condensed moisture in the stack and thus is a very Important variable to be
considered in the design of wet stack systems.  The validity  of these
laboratory measurements needs to be confirmed by comprehensive  field
measurements.
                                       226

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                                                        TABLE 8 WET STACK DESCRIPTION
N>
ro
Plant Number
      1

      2
      3


      4

      5

      6
      7
                             Entrainment Condition
                             Entralnment 1s  a big
                             probl an
                             Moderate entrainment
                             Noticeable  Entralnment
                             during:
                             - absorber  overload
                             - dirty demisters
                             - plugged drains
                             No known entrainment
                             No known entrainment
                             No known entrainment
                             Slight noticeable entrain-
                             ment during humid weather
No.
Units
2
1
2
2
2
2
2
Participate
Removal
VentuM
ESP
Venturi
ESP
ESP
ESP
ESP
Absorber
Mobile Bed
Mobile Bed
Venturi
Venturi
Venturi
Mobile Bed
Mobile Bed
I.D.
Fans
Dry
Dry
Wet
Wet
Wet
Dry
Dry
Secondary
Demlsters
None
None
Tried retro-
fitting 3 con-
figurations with
no success
Yes
Chevron 4-pass
Yes
Chevron 4-pass
None
None

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                                                      TABLE 9 STACK BREECHING DUCT DATA
                                                Stack  Data
Breeching Duct Data - Entrance to
             Stack
Plant
1
2
ro
ro
00 3
4
5
6
7
Height
50m
(165 ft)
183m
(600 ft)
290m
(950 ft)
119m
(390 ft)
104m
(340 ft)
244m
(800 ft)
137m
(450 ft)
Diameter
(base-top)
4.9m
(16 ft.)
5.9m
(19-1/2 ft)
5.8m
(19 ft)
8.8-7. 9m
(29-26ft)
8. 8-7. 9m
(29-26 ft)
13.4-7.9m
(44-26 ft)
3.4m
(11 ft)
Gas Velocity
(max)
7.6m/s
(25 ft/s)
27.4 m/s
(90 ft/s)
27.4 m/s
(90 ft/s*)
7.3m/s
(24 ft/s)
llm/s
(36 ft/s)
24.4 m/s
(80 ft/s)
30 m/s
(95 ft/s)
Gas Temperature
(average)
43.3°C
(110°F)
48.9°C
(120°F)
48.9°C
(120°F)
48.9°C
(120°F)
48.9°C
(120°F)
51.7°C
(125°F)
54.4°C
(130°F)
Liner Material
Carbon Steel
w/ Precrete
Mild steel w/
Ceil coat
Carbon Steel
w/ Heil Rigi-
flake
Acid proof
Brick & Mortar
Acid proof
Brick & Mortar
Acid Proof
Brick & Mortar
Acid Proof
Brick & Mortar
Liner
Insulation
None
2-3 Inches
fiberglass
None
None
None
None
None
No.
Flues
1
1
4
1
1
1
1
Height
Width
Scrubber & demlster
share stack flow
enters at bottom of
stack.
7.6m
(25 ft)
12.2m
(40 ft)
12.2m
(40 ft)
9.1m
(30 ft)
5.8m
(19 ft)
3.7m
(12 ft)
3.7m
(12 ft)
3.7m
(12 ft)
4.6m
(15 ft)
2.3m
(7-1/2
ft)
Distance from
dust to stack
exit
From demlster
23m
(75 ft)
247m
(810 ft)
88m
(290ft)
72m
(2325 ft)
213m
(700 ft)
101m
(330 ft)
* Secondary source gives 60 ft/sec velocity.

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FUTURE PROGRAM EMPHASIS


Future R&D emphasis will be on the following:

    o    Demonstrations

        « Chiyoda 121
        ~ RESOX
        — Aqueous carbonate process

    o    Pilot Plant

        — Absorption/steam stripping  improvements
        ~ Spray dryer testing
        — Integrated emission control

    o    Field Testing

        — Continuous emission monitor testing
        — Materials testing
        — Spray dryer chacterization

    o    Evaluations

        ~ Reliability improvements
        — Cyclic reheat feasibility

    o    Laboratory Testing

        -- Corrosion inhibitors
        -- Limestone dissolution
        -- Crystallization
        ~ Additives
                                        229

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         Tech Transfer

         -- Revised Lime FGD Systems Data Book
         — Issue limestone data book
         -- Continuous emission monitor guidelines
         — Workshops and seminars
CONCLUSION

EPRI research and development has attempted to address problems in FGD which
have led to the high cost,  low reliability and inefficient resource use in
current systems.  EPRI's efforts are aimed at near term solutions to problems
in system chemistry, corrosion, cost,  energy use,  by-product character, and
system design.  The results reported in this paper are documented more fully
in individual  reports that  are either  in print or  in the process of publica-
tion.  EPRI welcomes and encourages comments, criticisms ,or inquiry regarding
its FGD programs and asks that such calls be directed to Stu Dalton, Program
Manager, Desulfurization Processes Program.   (415) 855-2467.
                                         230

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Session 4:'UTILITY  APPLICATIONS
    H. William Elder, Chairman
    Tennessee Valley Authority
      Muscle Shoals, Alabama
                231

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         TEST  RESULTS  ON  ADIPIC  ACID-ENHANCED LIMESTONE SCRUBBING
                     AT THE  EPA SHAWNEE  TEST FACILITY
                              -THIRD  REPORT-

                D.A.  Burbank,  S.C.  Wang, and R. R.  McKinsey
                          Bechtel  National,  Inc.
                              50  Beale Street
                     San Francisco, California  94105

                                   and

                               J.E. Williams
               Industrial  Environmental  Research  Laboratory
                   U.S. Environmental  Protection  Agency
               Research Triangle  Park, North Carolina 27711


                                 ABSTRACT

Adipic acid has been  demonstrated as  a powerful scrubbing additive  for
enhancing SO? removal  in lime  and limestone  wet scrubbing tests  both
at the EPA/IERL pilot plant  at Research  Triangle  Park, North  Carolina,
and at the  EPA-sponsored Shawnee  Test Facility near Paducah,  Kentucky.
Improved limestone utilization and operating reliability have also  been
demonstrated.

Earlier test results  using adipic acid,  from July 1978 through October
1979, were  reported at the Fifth  Symposium on Flue  Gas Desulfurization
in Las Vegas, Nevada, March  5-8,  1979, and at EPA's Fifth Industry  Briefing
in Raleigh, North Carolina,  December  5,  1979.  This is the third report
on the recent adipic  acid  test results at the Shawnee Test Facility from
October 1979 through  May 1980.

The recent  tests with adipic acid were conducted  only on the  venturi/spray
tower system.  All  tests were  made with  limestone slurry.  These included:
(1) partial factorial  tests  to characterize  the effects  of pH, adipic  acid
concentration,  and other operating parameters on  S0? removal; (2)  single-
loop (one-tank) tests without  forced  oxidation at low pH and  high  (4000
ppm) adipic acid concentration; (3) tests with a  venturi only to determine
the limits  of SO? removal; (4) single-loop forced oxidation tests,  with
both one tank and two tanks; and  (5)  bleed stream oxidation tests  at low
pH and high (4000 ppm)  adipic  acid concentration.

Major efforts during  the recent test  period  were  directed toward investiga-
tion of the effect of pH on  the degradation  of adipic acid.  It was found
that the adipic acid  degradation  is minimized when  the scrubber is  operated
at low (below 5.0-5.1)   inlet  pH.   Forced oxidation and  poor  limestone utili-
zation tend to  increase the  deqradation.
   Preceding page blank
                                   233

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                              ACKNOWLEDGMENT
The authors wish to express their appreciation to the following Bechtel
personnel who contributed to the preparation of this paper:

                 C. L. DaMassa             H. K. Pate!
                 T. M. Martin              D. T. Rabb
                 D. P. McGrath             C. H. Rowland
                 M. S. Mihalik             V. C. Van der Mast

The authors wish to thank Gary Rochelle of the University of Texas at
Austin, consultant to the project, for his constant input of ideas and
assistance in the adipic acid development program.

Further acknowledgment and appreciation are extended to personnel of TVA's
Energy Design and Operations Branch, both at the Shawnee Test Facility
and in Muscle Shoals, Alabama, who are responsible for operation, main-
tenance, and engineering modification of the facility.

The contribution and support of the Department of Energy are also acknowledged.
                                   NOTE
Although it is the policy of the EPA to use the metric system for quantitative;
descriptions, the British system is used in this report.  Readers who are more
accustomed to metric units are referred to the conversion table in the Appendix;
                                      234

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                  TEST RESULTS ON ADIPIC  ACID-ENHANCED
                     LIMESTONE SCRUBBING  AT  THE  EPA
                          SHAWNEE TEST  FACILITY

                            - THIRD  REPORT -
                                Section  1

                               INTRODUCTION
Since October 1977 one  of  the  primary objectives  of the  Environmental  Protection
Agency (EPA) alkali wet scrubbing  test program has been  to enhance  S02 removal
and improve the reliability  and  economics  of the  lime and limestone wet scrubbing
systems by use of adipic acid  as a chemical  additive.

Testing of adipic acid-enhanced  limestone  scrubbing began in  October 1977  at
the EPA 0.1 MW pilot  plant at  Industrial  Environmental  Research  Laboratory,
Research Triangle Park  (IERL-RTP), North  Carolina (Reference  1).  As a logical   ;
progression, larger scale  testing  was conducted beginning in  July 1978 at  EPA's  10
MW prototype Shawnee  Test  Facility located at the Tennessee Valley  Authority (TVA)
Shawnee Steam Plant near Paducah,  Kentucky.   Test results from the  Shawnee Test
Facility from July 1978 through  October 1979 were presented in two  previous  reports
(References 2 and 3).   As  part of  EPA's continuing program of technology transfer.,
to further demonstrate  the effectiveness  of adipic acid, and  to  encourage  its  use,
the EPA contracted with Radian Corporation in the spring of 1980 to carry  out  a
full-scale demonstration program of adipic acid-enhanced limestone  scrubbing.  The
program is being conducted at  the  Springfield City Utilities'  Southwest Station
near Springfield, Missouri.  Testing in the full-scale units  began  in the  late
summer of 1980.

This report is the third presenting the test results with adipic acid from the
Shawnee Test Facility.   The  report covers  the period from October 1979 through Mcy
1980.  During this period, adipic  acid testing was conducted  only on the venturi/
spray tower system  (Train  100).  All  tests were conducted with limestone slurry
and with flue gas having high  fly  ash loading (3  to 6 grains/scf dry).

During the report period,  Train  200 (TCA)  was operated by EPRI/UOP/TVA on  a
DOWA basic aluminum sulfate  process, and Train 300 was operated  by  EPRI/TVA
on a cocurrent, high-velocity  scrubber configuration.
THEORY  AND  ADVANTAGES  OF  ADIPIC  ACID-ENHANCED SCRUBBING

Adipic  acid is  a  dicarboxylic  organic acid [HOOC(CH2)4COOH] in powder form,
which is  commercially  available  and used primarily as a raw material  in
the nylon manufacturing industry.   Initial tests with adipic acid at the
                                       235

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IERL-RTP pilot plant were undertaken as a result of theoretical analyses by
Rochelle (Reference 4).  Adipic acid effectively buffers the pH in limestone/
lime SOo absorbers and improves the S02 removal efficiency.  The buffering
action limits the drop in pH at the gas/liquid interface during S02 absorp-
tion, and the resultant higher concentration of S02 at the interface accele-
rates the liquid-phase mass transfer.  The capacity of the bulk liquor for
reaction with S02 is also increased by the presence of calcium adipate in
solution.  Thus, the S02 absorption becomes less dependent on the dissolution
rate of limestone or CaSOo in the absorber to provide the necessary alkalinity.
In the case of limestone scrubbing, it follows that a given S02 removal effi-
ciency can be achieved at a lower limestone stoichiometry.

Further analysis by Rochelle (Reference 5) suggested that the use of additives
would be most attractive economically when used in scrubbers employing forced
oxidation.  If no decomposition or volatilization of the additive occurs, the
makeup requirements of the additive would be minimized by the more tightly
closed liquor loop achievable due to the better dewatering properties of the
oxidized sludge.

Several advantages of adipic acid over other additives, such as MgO, have been
cited previously (References 1, 2, and 3).  Further, the optimum concentration
of adipic acid for effective improvement in S02 removal is only 700 to 1500 ppm
at a scrubber inlet pH above about 5.2.  The preliminary economic evaluations
(Reference 2) have shown that adipic acid can reduce both the capital investment
and the operating cost of limestone systems while simultaneously increasing the
performance, even under those conditions in which the actual addition rate is
3 to 5 times the theoretical requirement due to the degradation of the acid.

This report shows that the degradation of adipic acid can be minimized when the
scrubber inlet pH is lowered to below about 5.0.  Although higher adipic acid
concentration is needed at the lower pH to achieve the same degree of S02 removal
efficiency, overall adipic acid consumption is reduced compared to the higher pH
operation.  For this reason, and with the further improvement in limestone utili-
zation at low pH, the low pH operation should be more economically attractive.
Section 11 presents an update of the economic evaluations given in Reference 2.
TEST FACILITY AND PROGRAM

Readers who are unfamiliar with the Shawnee Test Facility and the earlier adipic
acid test programs are referred to References 2 and 3.  A summary of the earlier
work is given in Section 2.  This report covers the adipic acid test results from
October 1979 through May 1980 on the venturi/spray tower system.  The following
adipic acid tests were conducted during this period:

     *  Partial  factorial  tests to characterize the venturi/spray tower
        performance using a single tank without forced oxidation

     •  Investigation of the effect of pH on adipic acid degradation
        with and without forced oxidation
                                       236

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    t  SOg  removal  capability of the venturl scrubber alone

    •  Forced  oxidation  within the scrubber loop using a single tank

    •  Forced  oxidation  within the scrubber loop using two tanks in series

    t  Forced  oxidation  of the bleed stream


All tests were  conducted  using limestone slurry and flue gas containing 3 to 6
grains/dry scf  of fly ash.   Sections 3 to 8 discuss and summarize these tests.

Section 9 describes  scrubber system behavior during limestone blinding and
the conditions  leading to it.  Recommended solutions for eliminating or
avoiding limestone blinding are also given.  Section 10 gives updated data
on the dewatering properties of adipic acid-enhanced limestone slurry.
                                       237

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                                 Section 2

                         SUMMARY OF PREVIOUS WORK
Based on the earlier test results through October 1979 (References 1, 2 and 3),
both at the IERL-RTP pilot plant and at the Shawnee Test Facility, the charac-
teristics of adipic acid as a lime/limestone scrubber additive can be summarized
as follows:


BENEFICIAL ASPECTS

     ®  Adipic acid significantly enhances SOo removal.  At a scrubber inlet
        pH above about 5.2, at which most of the adipic acid is in ionized
        form, the optimum concentration range is only 700 to 1500 ppm.

     •  At the minimum effective pH of 5.2, the corresponding limestone
        utilization is normally about 80 percent or higher; thus the quantity
        of waste solids generated is reduced.  High limestone utilization
        also contributes to reliable scrubber operation.

     «  With proper pH control  and sufficient adipic acid concentration
        (sufficient buffer capacity), steady outlet S02 concentrations can
        be maintained even with wide fluctuations of inlet S02 concentrations.

     •  Adipic acid-enhanced limestone scrubbing has lower projected capital
        and operating costs than unenhanced limestone or limestone/MgO scrubbing
        (Reference 2).  This is primarily due to the reduced limestone consump-
        tion, the associated grinding cost, and the reduced quantity of waste
        sludge generated with adipic acid-enhanced scrubbing.

     «  Since limestone dissolution is not a rate-controlling step in S02
        absorption for an adipic acid-enhanced limestone system, adipic
        acid should promote use of less expensive and less energy-intensive
        limestone than lime.

     «  The effectiveness of adipic acid is not affected by forced oxidation
        and it can be used with both lime and limestone in systems with or
        without forced oxidation.

     •  The effectiveness of adipic acid is not adversely affected by chlorides
        as is the 1imestone/MgO process.  Thus it is especially attractive for
        very tightly closed liquor-loop operation.

     «  When used with lime, both good S02 removal and sulfite oxidation can
        be achieved in a single-loop scrubbing system using within-scrubber-
        loop forced oxidation.


NEGATIVE ASPECTS

     »  Adipic acid decomposition, and the indications of its being adsorbed
        on solids or occluded in solids (Reference 6), require adding up to

                                      238

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       5 times that amount theoretically  required  (Reference  2).   However,
       the consumption over the  ranges  anticipated has  negligible  economic
       impact.

    •  Some decomposition products,  such  as  valeric acid,  have  an  unpleasant
       odor.  However, this has  not  been  a problem in testing to date.


OTHER CONSIDERATIONS

Tpxicity.  No further work in  this  area  has been  conducted  by  the EPA  since
the last report (Reference 3).  Preliminary results from Level 1 chemical
and bioassay analyses showed no measurable difference in toxicity or mutage-
nicity  of samples with and without  adipic  acid  addition. These  samples were
taken in February 1979 from a  limestone/adipic  acid forced-oxidation run  and
a base  case limestone run without forced oxidation.  It  should be noted that
adipic  acid is a food additive.

Limestone Blinding  and Calcium Sulfite Scaling.   Adipic  acid buffers the  pH
drop across the scrubber, and  therefore  increases the potential  of  calcium
sulfite scaling at  the bottom  part  of the  scrubber.  At  a constant  liquid-to-
gas ratio, addition of adipic  acid  increases  the  S02 make-per-pass  and
similarly increases the sulfite scaling  tendency  at the  bottom of the  scrubber.
In the  case of limestone  scrubbing, blinding  of limestone by calcium sulfite
could occur, resulting in low  pH  and  poor  limestone utilization.  This would
be particularly true with forced  oxidation in the scrubber  loop  (or in a
system  with a high  level  of natural oxidation);  such conditions  deplete calcium
sulfite solid seeds.  Operating and design considerations for  avoiding limestone
blinding are presented in Section 9.
                                       239

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                                 Section 3

                FACTORIAL  TESTS  ON  THE  VENTURI/SPRAY TOWER
                 SYSTEM WITH LIMESTONE/ADIPIC ACID SLURRY
Fifty 1 linestone/adipic acid partial  factorial  tests,  Runs VAA201 through
VAA250,  were conducted on the venturi/spray tower system.  All  tests were
made without forced  oxidation and with  a  common effluent hold tank as shown
in Figure 3-1.

The tests examined the effect of spray  tower liquid-to-gas ratio, scrubber
inlet liquor pH, and adipic acid concentration on S02 removal.   Table 3-1
summarizes the test results.   The operating conditions held constant during
these tests were:

          Fly ash loading:   High (3-6 grains/dry scf)
          Flue gas rate:   35,000 acfm @ 300°F  (except Run VAA 207 @ 20,000 acfm)
          Hold tank level:   8 ft 6 in.  (9.1 -  38 minutes residence time)
          Slurry solids concentration:  15 percent
          Venturi pressure drop:  9 inches H20 for runs with 600 gpm,
                     plug wide open for runs with 125 gpm
          Spray header configuration (top header is No. 4):
                     For  400 gpm	Header  4
                     For  800 gpm 	  Headers 3 and  4
                     For 1200 gpm 	  Headers 2,3, and 4
                     For 1600 gpm 	  All four headers
          Solids dewatering equipment:  Clarifier and centrifuge


OVERALL S02 REMOVAL  BY VENTURI AND SPRAY  TOWER

Equation 3-1 for predicting S02 removal has been fitted to the 10 venturi/spray
tower runs (Runs VAA201 through VAA206  and VAA234 through VAA237) for which the
slurry flow rate to  the venturi was held  at 600 gpm and the venturi pressure
drop was 9 inches H20.

     Fraction S02
     Removal       = 1 -  exp  [-0.0019  (L/G)0'55 exp(0.8pH + 8xlO'4 A}]  (3-1)

       where:
              L/G =  spray tower liquid-to-gas  ratio,  gal/mcf (saturated)
              pH  =  scrubber  inlet liquor pH
              A   =  adipic  acid concentration  in scrubber liquor, pprc

The ranges of operating variables covered by the 10 correlated runs are:

                             L/G  =  15-57 gal/mcf
                              pH  = 5.2-5.8 (limestone stoichiometry
                                    controlled at 1.2)
                               A  = 600-1400  ppm
                  Gas flow rate  = 35,000 acfm at 300°F
         Inlet S02 concentration  = 1500-2200 ppm

                                      240

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                                            MAKEUP WATER
                                                         CLARIFIED LIQUOR FROM
                                                        SOLIDS DEWATERING SYSTEM
                                                            BLEED TO SOLIDS
                                                          DEWATERING SYSTEM
G-104
      Figure 3-1.   Flow Diagram  for the  Venturl/Spray Tower  System
                     With One Tank and Without Forced  Oxidation

-------
                                                            Table  3-1
                                      RESULTS  OF LIMESTONE/ADIPIC ACID  FACTORIAL  TESTING
                            ON THE  VENTURI/SPRAY TOWER USING ONE TANK  WITHOUT  FORCED OXIDATION
Run
Mo.
VAA201
VAA202
YAA203
VAA204
VAA205
VAA206
VAA207
VAA208
VAA209
VAA210
VAA211
VAA21-2
VAA213
VAA214
VAA215
VAA216
VAA217
VAA218
VAA219
VAA220
VAA221
VAA222
VAA223
VAA224
VAA225
VAA226
VAA227
VAA228
VAA229
VAA230
VAA231
VAA232
VAA233
VAA234
VAA235
VAA236
VAA237
VAA23S
VAA239
VAA240
VAA241
VAA242
VAA243
VAA244
VAA245
VAA246
VAA247
VAA248
VAA249
VAA250
Liquor Rate
(qpm)
Venturl ST
600 1200
600 800
600 400
600 1600
600 800
600 1200
125 1200
125 800
125 1200
125 400
125 1600
125 1200
125 800
125 1200
125 1200
125 1200
125 1600
125 1600
125 1200
125 1600
125 800
125 400
125 1200
125 1600
125 800
125 400
125 1200
125 1200
125 1200
125 800
125 800
125 1200
125 800
600 800
600 400
600 1200
600 800
125 800
125 1200
125 400
125 1600
125 800
125 1200
125 400
125 800
125 800
125 800
125 1200
125 1200
125 1200
ST
L/G
(gal/mcf)
43
29
15
57
29
43
75(1>
29
43
15
57
43
29
43
43
43
57
57
43
57
29
15
43
57
29
15
43
43
43
29
29
43
29
29
15
43
29
29
43
15
57
29
43
15
29
28
29
43
43
43
Pressm
(Inch
Venturl
8.9
8.7
8.8
8.9
8.9
8.7
0.9
2.3
3.1
2.4
3.7
2.fi
2.5
3.1
2.7
2.7
2.7
2.3
2.6
2.7
1.9
3.3
3.0
3.4
3.1
4.0
3.1
3.6
3.7
4.6
4.1
4.2
3.9
9.0
9.2
8.9
9.0
3.1
3.2
3.7
3.7
3.1
2.9
3.R
3.0
3.0
3.8
2.9
3.0
3.8
•e Drop
H,0)
Total
13.5
14.4
13.6
14.1
15.0
14.6
3.1
7.7
7.9
7.0
8.8
7.9
7.7
8.6
9.0
8.1
7.7
7.6
8.0
7.4
8.6
7.9
7.8
8.2
7.9
9.0
8.0
8.9
8.9
9.7
9.6
8.9
8.9
14.0
15.2
12.2
11.3
8.1
8.1
8.5
9.3
7.6
7.7
8.6
7.5
7.9
9.0
7.7
7.7
9.2
Inlet
Liquor
PH
5.70
5.45
5.85
5.75
5.80
5.65
5.75
5.85
5.70
5.80
5.85
5.60
5.65
S.35
5.05
4.65
5.35
5.00
5.00
4. 300°F for Run VAA207.
                                • C« 300°F.

-------
    Venturl Hqu1d-to-gas ratio  •   21  gal/mcf
          Venturl pressure drop  •   9 Inches  H20

Equation 3-1 explains 90 percent of the  variation  in  the  data  for S02  removal
with a standard error of estimate of  2.7  percent S02  removal  (see Figure 3-2)
S02 REMOVAL BY SPRAY TOWER ONLY

Equation 3-2 for prediction of S02  removal  has  been  fitted  to  the 40  spray
tower runs (minimum effect of venturi  -  125 gpm for  flue  gas humidification):

     Fraction S02
     Removal       = 1  - exp [-2.2xlO~4  (L/G)0'75  exp  (pH + 6.2xlO~4  A)]   (3-2)

where L/G, pH, and A have the same  definitions  as  for  Equation 3-1.

The ranges of variables covered  by  the 40  correlated runs are:

                          L/G   =   15-75 gal/mcf
                           pH   =   4.6-5.9
                            A   =   600-2400 ppm
                Gas flow rate   =   35,000  acfm  at  300°F  (one test at  20,000  acfm)
        Inlet S02 concentration  =   1600-2900 ppm
       Venturi slurry  flow rate  =   125 gpm
        Venturi pressure drop   =   2-4 inches H20  (wide  open plug)

Equation 3-2 explains  93 percent of the  variation  in the  data  for S02 removal
with a standard error  of estimate of 4.3 percent S02 removal (see Figure  3-3).
It is important to note that the S02 removal  predicted by Equation  3-2
includes the effect of the venturi  operating at the  minimum conditions defined
above. The magnitude  of this effect is  discussed  later.

Figures 3-4 through 3-6 illustrate  the effects  of  spray  tower  liquid-to-gas
ratio and inlet liquor pH on S02 removal at adipic acid  concentrations of
600, 1300, and 2000 ppm, respectively.  The lines  on the  figures represent
the predictions of Equation 3-2  with actual data points  also shown.

Note that the S02 removals for a pH of 4.6 and  2000  ppm  adipic acid in
Figure 3-6 are similar both to those in  Figure  3-5 for a pH of 5.0  and 1300  ppm
adipic acid, and to those in Figure 3-4  for a pH of  5.4  and 600  ppm adipic
acid.  These values are more clearly seen  in the following:

                                           Percent S02 Removal at
       Scrubber        Adipic                 Spray Tower L/G of
        Inlet          Acid,
         pH            ppm

         5.4            600

         5.0           1300

         4.6           2000
30 gal/mcf
60
61
62
243
50 gal/mcf
74
75
76

70 gal/mcf
82
83
84


-------
     100
       70
                                                     100
                    MEASURED PERCENT SO2 REMOVAL
Figure 3-2.   Measured vs.  Predicted  (Eq.  3-1) S02  Removal
              by the Venturi/Spray Tower
                                             90
                                                     100
                    MEASURED PERCENT SO2 REMOVAL
 Figure 3-3.  Measured vs.  Predicted  (Eq.  3-2) S0?  Removal
              by  the.Spray  Tower
                            244

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                   20
                           30      40       SO      60


                          LIQUID-TO-GAS RATIO, gel/mrf (uturatad)
                                                         70
                                                                80
Figure  3-4.   Effect of Spray Tower  Liquid-to-Gas Ratio and Inlet pH
              on  Spray Tower S02 Removal at  600 ppm Adi pic Acid
          100
                                               ApH-5.7
                                               QpH-5.4
                                               VPH-5.0
                                               D pH - 4.6
                          LIQUID-TO-GAS RATIO, gal/mcf (saturated)
Figure  3-5.  Effect of  Spray Tower Liquid-to-Gas  Ratio and  Inlet pH
              on  Spray Tower SO?  Removal at 1300 ppm Adi pic  Acid
                                     245

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i
UJ
cc


S
i-

UJ
O
K
ut
a.
                                               ApH = 5.7

                                               O pH = 5.4

                                               V pH = 5.0

                                               D pH = 4.6
                         30        40         50        60




                      LIQUID-TO-GAS RATIO, gal/mcf (saturated)
    Figure 3-6.   Effect  of Spray Tower Liquid-to-Gas  Ratio and  Inlet

                  pH on Spray Tower  S02 Removal  at 2000 ppm Adipic Acid
                                       246

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Thus, within the ranges  tested,  each 0.4 unit drop in scrubber inlet pH
requires a 700 ppm  increase  in  adipic acid concentration to achieve similar
percent S02 removal.


S02 REMOVAL BY VENTURI ALONE AT MINIMUM SLURRY FLOW RATE AND PRESSURE DROP

For a 2 to 4 hour period at  the end of each of seven factorial  tests
with the spray tower  alone (Runs VAA210, VAA213,  VAA222, VAA231,  VAA238,
VAA239, and VAA240),  the spray  tower slurry flow was shut off in  order to
determine the S0£ removal  achieved by the venturi alone at a minimum slurry
flow rate of 125 gpm, minimum pressure drop of 2 to 4 inches H?0  (wide open
plug), and 35,000 acfm gas flow rate (venturi L/G = 4.5 gal/mcf).  These
tests  indicated that, at these  conditions, the venturi scrubber obtains about
20 percent S02 removal at 600 ppm adipic acid concentration and an inlet  pH
of 5.7, 22 percent  SO?  removal  at 1300 ppm adipic acid and a pH of 5.3, and 42
percent S02 removal  at 2000  ppm adipic acid and a pH of 5.4.  Equation 3-2
does not  Include any  corrections for SOo removal  in the venturi.   This should
be taken  Into consideration  when using Equation 3-2 with Figures  3-3
through 3-6.
                                       247

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                                 Section  4

                  EFFECT  OF  pH  ON ADIPIC  ACID  CONSUMPTION
During both the earlier factorial  tests  with  adipic acid addition (Reference
3) and the latest factorial  tests  (Section  3),  it was noticed that the
rate of adipic acid addition required to maintain a desired concentration  in
the scrubber liquor was substantially reduced when the scrubber inlet pH was
controlled at 5.0 or lower.   At higher pH operation,  it is necessary to add
adipic acid at up to about 5 times the theoretical  addition rate (as defined
below), either because of degradation or decomposition of the adipic acid.
Apparently, the degradation  or decomposition  process  is inhibited under low
pH conditions.

Although the exact mechanism of adipic acid degradation is still  not under-
stood, it was decided to investigate  the effect of pH on the adipic acid
consumption rate in more detail.

Early in the adipic acid-enhanced  lime/limestone testing,  it was noted that
the S02 removal  enhancement  by the adipic acid  is maximized when the scrubber
inlet pH is maintained at about 5.2 or higher under the prevailing scrubber
conditions (chloride concentrations).  This is  because most of the adipic  acid
is ionized and its buffering capacity more  fully utilized at these higher
inlet pH levels (Reference 7).

Operations at lower pH therefore require higher adipic acid concentrations
to maintain the same degree  of S02 removal  efficiency (Section 3), because
the ionization and buffer capacity of adipic  acid are reduced.  However,
experience at Shawnee shows  that the  total  adipic acid consumption at a
scrubber inlet pH below 5.0  and concentration as high as 4000 ppm is actually
lower than at a pH of about  5.4 and 1500 ppm  when significant degradation  was
noted.  Potential advantages of low pH operations are obvious:

     •  Lower operating cost due to lower adipic acid consumption.

     •  Easier forced oxidation, in-loop or bleed stream, and less air (and
        compressor energy).

     0  Essentially complete limestone utilization and improved scrubber
        operating reliability.

     •  Reduced sensitivity  to limestone type and grind; fine grinding of
        limestone is probably not  required.

     «  Lower sulfite scaling potential.

     0  Better prospects (sensitivity) for  automatic  pH control.

     •  Greater flexibility  for S02 emission  control; high sensitivity of
        S02 removal  to pH allows raising p'H to  increase the buffer capacity
        and S02 removal  when needed.


                                      248

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    •  Improved acceptance of the concept by  plant  owners  because  of  the
       reduced quantity of adlplc add degradation  products.

    •  Applicability to low-sulfur  subbituminous  and  lignite  coals containing
       alkaline ashes which are extractable only  at low  pH.

    •  Probable lower cost due to all of the  above  factors.
Seven  runs were conducted on  the venturi/spray  tower  system  to  investigate
the effect of pH on the  adipic  acid  consumption rate.   These tests were made
with a single effluent hold tank and without  forced oxidation.  The  flow
configuration for these  tests is the same  as  that shown in Figure 3-1.
DISCUSSION OF TEST  RESULTS

Table 4-1 summarizes  the  major test conditions  and  the  run-average  results
for the  seven tests made  in  this  series.   The  scrubber  inlet  pH  and the  adipic
acid concentration  were varied in the  tests.   All other conditions  were  held
constant.

Theoretical  Adipic  Acid Consumption Rate.    The theoretical adipic  acid
consumption  rate  is defined  as the rate of adipic acid  leaving the  scrubber
system in the liquor  which is entrained in the  discharged sludge (filter
cake, centrifuge  cake, or clarifier underflow)  in a closed-liquor-loop
operation.   The theoretical  consumption rate is calculated from  the material
balances for solids discharged from the scrubber system, solids  (or liquor)
concentration in  the  discharged sludge, and adipic  acid concentration  in the
liquor.

Since some adipic acid decomposes to lower-carbon carboxylic  acids  and  the
analytical method employed at the Shawnee  laboratory determines  the total
carboxyl group, "adipic acid concentration" as  reported throughout  this
report means "total carboxylic acid expressed  as adipic acid."   Note that
most of the  degradation products  are also  effective as  enhancing agents  for
SO2 removal.

Effect of pH on Adipic Acid  Consumption Rate.   As can be seen in Table  4-1,
the ratios of actual-to-theoretical adipic acid consumption were all 1.0 at
a scrubber inlet  pH of 4.60  and 4.85 for Runs  926-1A, 926-1G, and 926-1B,
when the adipic acid  concentrations were controlled at  4090,  2270,  and  1435
ppm; respectively.  This  indicates that there  was essentially no degradation
of adlpic acid, within the accuracy of the material balance calculations.

Further increase  in the scrubber  inlet pH  to 5.05,  5.25, and  5.50 during Runs
926-1C,  926-1H, and 926-1D resulted in actual-to-theoretical  adipic acid
consumption  ratios  of 1.17,  1.24, and  1.59, respectively.

Despite  the  higher  adipic acid concentration required at the  lower  pH  operation,
the total adipic  acid consumption can  be actually less, as can be seen  in
Table 4-1, in terms of actual  adipic acid  consumption per ton of SO^ absorbed.


                                      249

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                                                          Table 4-1
                                  RESULTS OF VENTURI/SPRAY TOWER LIMESTQNE/ADIPIC  ACID
                                   TESTS USING A SINGLE TANK WITHOUT FORCED OXIDATION
Major Test Conditions
Fly ash loading
Gas rate, acfm'e 300°F
Venturi liquor rate, gpm
Spray tower liquor rate, gpm
Percent solids recirculated (controlled)
EHT residence time, m1n
EHT tank level, ft
Scrubber inlet pH (controlled)
Adipic acid concentration, ppm
Venturi pressure drop, Inches HoO
Run-Average Results
Start-of-run date
Onstream hours
Percent SO^ removal
Inlet S02 concentration, ppm
Adipic acid concentration, ppm
Actual adipic acid consumption, Ibs/tons S0£ abs.
Adipic acid consumption ratio ( actual /theor)
Percent solids recirculated
Scrubber Inlet pH
Scrubber outlet pH
SO^ make-per-pass, mmole/1
Limestone utilization, %
Scrubber Inlet sulfite concentration, ppm
Scrubber outlet sulfite concentration, ppm
Sulfite oxidation, %
Scrubber inlet gypsum saturation, %
Centrifuge cake solids, wt%
Mist eliminator restriction, %
926-1A
High
35,000
600
1600
15
9.1
8.5
4.6
(1)
9

12/18/79
297
90
2650
4090
—
1.0
15.5
4.60
4.30
8.05
97
1540
1550
49
130
69

926-1G
High
35,000
600
1600
15
9.1
8.5
4.8
(1)
9

1/3/80
244
91
2250
2270
4.3
1.0
15.1
4.85
4.50
6.90
96
875
1440
51
116
70

926-1 B
Hiqh
35,000
600
1600
15
9.1
fi.5
4.8
1300
9

1/16/flO
184
84
2115
1435
3.0
1.0
14.9
4.85
4.55
6.00
95
965
1545
49
127
69
0
926-1 C
Hiqh
35,000
600
1600
15
9.1 ,
8.5
5.0
1300
9

1/24/PO
116
91
2150
1290
5.7
1.17
15.1
5.05
4.65
6.60
95
325
695
47
129
66

926-1H
High
35,000
600
1600
15
9.1
8.5
5.25
1300
9

1/29/80
169
93
2150
1285
8.0
1.24
14.9
5.25
4.85
6.75
92
180
305
30
118
61

926-10
Hiqh
35,000
600
1600
15
9.1
8.5
5.5
1300
9

2/8/80
116
96.5
2410
1330
9.6
1.59
15.5
5.50
5.00
7.85
80
135
185
17
112
60

926-1 E
Hiqh
35,000
600
1600
15
9.1
8.5
5.0
700
9

2/15/80
119
77
2450
735
6.0
1.0
15.2
5.05
4.60
6.35
95
325
710
32
113
60
0
on
O
      Notes:  (1)  Adipic acid concentration controlled at a level to provide 92% S02 removal.

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Effect of  pH  and Adipic Acid  Concentration  on SO?  Removal.   As mentioned  in
Section 3,  the  results of  factorial  tests show that higher  adipic  acid con-
centration  is required at  low pH  than  at high pH  to achieve similar  S02 removal.
This trend  is also  evident from the  results of Runs 926-1A,  926-1G,  926-1C and
926-1H:

                                    926-1A    926-1G     926-1C    926-1H

   Scrubber inlet pH                   4.60      4.85     5.05      5.25
   Adipic  acid  cone., ppm              4090      2270     1290      1285
   Percent S02  removal                  90         91      91         93
   Inlet SO?  cone., ppm                2650      2250     2150      2150
   Percent limestone  utilization        97         96      95         92

Thus, the  optimum scrubber inlet  pH  appears to be  5.0  to  5.1  (Run  926-1C) where
adipic acid concentration  required is  only  about  1300  ppm to  achieve 91 percent
S02 removal.  More  importantly, the  adipic  acid degradation is insignificant
at this pH level  (1.17 actual-to-theoretical  consumption  ratio for Run 926-1C).

Note that  S02 removal is more sensitive to  pH and  inlet. S02 concentrations at
the scrubber inlet  pH levels  of 4.6  to 4.85 tested because  the buffer capacity
of adipic  acid  is reduced  at  the  lower pH levels.

Limestone  Utilization.  One of the benefits of the low pH operation  is that
very high  limestone utilization can  be realized.   Limestone utilizations
were 95 percent or  higher  at  the  scrubber inlet pH of  5.05  or lower  and
9.1 minutes residence time in the effluent  hold tank.

Sulfite Oxidation and Centrifuge  Cake  Solids.  Another important benefit  of
low pH operation is the ease  of  forced oxidation  of sulfite.  A  natural
oxidation  level of  about 50 percent  was achieved  at the scrubber inlet pH of
5.05 or lower,  as compared to 15  to  20 percent oxidation  at a normal inlet
pH of about 5.5.  The resulting centrifuge  cake solids concentrations were
almost 10  percentage  points higher for the  lower  pH operation.
SUMMARY

The following is a summary of the test results:

     •  Apparent degradation of adipic acid is inhibited at low pH,  with  or
        without forced oxidation (see Sections 6 and 7).  Without forced
        oxidition, the critical  pH appears to be about 5.0 at the scrubber
        inlet,  below which degradation is minimized (actual-to-theoretical
        consumption ratio equals 1.0).

     •  Because of reduced ionization and buffer capacity of acipic  acid  at low
        pH, the required adipic acid concentration is 2 to 3 times higher at a
        scrubber inlet pH of 4»6 to 4.85 than at 5.05 to 5.25 to achieve  a similar
        degree  of S02 removal  (about 91 percent).

     •  Operation at low pH and high adipic acid concentration results in lower
        total adipic acid consumption than at high pH and low concentration.
                                       251

-------
•  The optimum scrubber inlet pH for the venturi/spray tower with a single-
   tank configuration appears to be 5.0 to 5.1 with respect to total adipfc
   acid consumption, limestone utilization, and the sensitivity of SOo
   removal  to pH and inlet S02 concentration.

e  Other benefits obtained when the scrubber inlet pH was held at 5.05 or
   lower include:  high limestone utilization (95 percent or higher),
   high natural  sulfite oxidation (about 50 percent), and the resultant
   high centrifuge cake solids (near 70 percent).
                                 252

-------
                                 Section  5

                       VENTURI  SCRUBBER S0?  REMOVAL
                    WITH LIMESTONE/ADIPIC ACID  SLURRY
A series  of  12  runs  (Runs  927-1A through  927-1L)  were made using  only  the
venturi scrubber  to  determine its maximum S02 removal capability  with  adipic
acid-enhanced limestone  scrubbing.

While.it  is  recognized that S02  removal with the  venturi  alone  would not meet
the S02 emission  standard  for high-sulfur coal, even with very  high concentra-
tions of  adipic acid, scrubbing  with the  venturi  alone could be attractive
economically for  low-sulfur coal  applications where only  70 percent S02
removal is required.

A single  tank was used without forced oxidation  for all  tests.  The flow
configuration for these  tests is the same as that shown in Figure 3-1,
except the slurry flow to  the spray tower (Pumps  G-101 and G-204) was  turned
off.

The slurry flow to the venturi was held constant  at 600 gpm for all runs.
Variables investigated were adipic acid concentration, gas rate (or venturi
liquid-to-gas ratio  at a constant slurry  flow rate), venturi pressure  drop,
and inlet pH.   Operating conditions common for all  runs were:

       Fly  ash loading:  High (3-6 grains/dry scf)
       Effluent  hold tank level:  8.5 ft
       Effluent  hold tank residence time:  33.4  minutes
       Slurry  solids concentration:  15  percent
       Solids  dewatering  equipment:  Clarifier  and centrifuge
DISCUSSION OF TEST RESULTS

Table 5-1 summarizes the major test conditions and the run-average test
results.

Effect of Adipic Acid Concentration.  Runs 927-1A, 927-1D, and 927-1E were
an operated at a gas rate of 35,000 acfm (@ 300°F), a liquid-to-gas ratio
of 21 gal/mcf, a venturi Inlet pH of 5.1, and at a pressure drop of about
8.3 Inches H20.  Average S02 removal increased from 34 to 41 and 65 percent
when the adipic acid concentration was raised from 815 to 1335 and 3985 ppm,
respectively.  Hourly S02 removal data for these three runs are plotted in
Figure 5rl.  It appears that the S02 removal levels off at about 65 percent,
suggesting that the overall  rate of S02 absorption may have been limited by
the gas-phase mass transfer above 3500 ppm adipic add.

Effect of Llquid-to-Gas Ratio.  During Runs 927-1B, 927-1C, and 927-1G, the
Tiquld-to-gas ratio was increased to 37 gal/mcf.  Average S02 removal increased
only marginally to 39, 47, and 68 percent, respectively.  For these runs,
venturi pressure drop was 6 inches H20.

                                       253

-------
                                                                                                    Table  5-1

                                                RESULTS  OF  VENTURI  LIMESTONE/ADIPIC  ACID   TESTS  USING  A  SINGLE  TANK
                                                                                     WITHOUT  FORCED  OXIDATION
X
              Major Test Conditions

              Fly ash loading
              Gas rate, acftn 0 300T
              Veoturl liquor rate, gpm
              Percent solids redrculat^d (controlled)
              EHT residence time, rain
              EHI tank level, ft
              Venturi inlet Ifouor pH (controlled!
              Adipic acid concentration, ppra
              Venturi pressure drop, Inches HUG
Run-Average Results

Start-of-run date
Onstreaoi hours
Percent S02 removal
Inlet S02 concentration, ppm
Adipic acid concentration, ppm
Scrubber percent solids reclrculated
Scrubber inlet pH
Sulfite concentration  in Inlet liquor, ppm
SO,  Hdke-per-pass, nwle/1
Linestone utilization, %
Sulfite oxidation, I
Inlet liquor gjpsura saturation, I
Centrifuge cake solids, wtt
Hist eliminator restriction, %
Ventur! pressure drop. Inches H?0
927-1A

 High
35,000
 600
 15
 33.4
 8.5
 5.1
 700
  6
2/JO/30
 43
 3«
 19QO
 B15
 14.6
 5.05
 365
 8.35
 92
 36
 115
 66

 8.2
927-18

 Hlqh
20,000
 600
 15
 33. 4
 8.5
 5.1
 700
  F
2/22/80
  24
  39
  2470
  705
  14.5
  5.15
  365
  6.80
  92
  34
  115
  67

  5.9
927-1J

 Hiqh
27.500
 600
 15
 33.4
 8.5
 5.1
 700
z/22/80
  24
  33
  2390
  795
  14.6
  5.10
  110
  7.65
  91
  29
  135
  68

  5.9
927-1C

 Hi oh
20,000
 600
 15
 33.4
 8.5
 5.1
 1300
  6
2/24/80
  48
  47
  2595
  1360
  14.0
  5.15
  330
  8.65
  91
  32
  120
  66

  6.0
                          927-10

                           High
                          35,000
                           600
                           15
                           33.4
                           8.5
                           5.1
                           1300
                            6
                         2/26/80
                          11
                          41
                          2445
                          1335
                          16.3
                          5.15
                          255
                          12.4
                          83
                          32
                          120
                          68

                          8.4
                                                   927-1E

                                                    High
                                                   35.000
                                                    600
                                                    15
                                                    33.4
                                                    8.5
                                                    5.1
                                                    4000
                                                    6
                                                 2/27/80
                                                   69
                                                   65
                                                   2360
                                                   3985
                                                   16.4
                                                   5.10
                                                   285
                                                   19.0
                                                   85
                                                   28
                                                   125
                                                   61

                                                   8.3
                                                                           927-1F

                                                                           Hi in
                                                                           27,500
                                                                           600
                                                                           15
                                                                           33.4
                                                                           8.5
                                                                           5.1
                                                                           4000
                                                                            6
                                                                           3/1/80
                                                                            26
                                                                            67("
                                                                            2255
                                                                            3990
                                                                            15.3
                                                                            5.10
                                                                            460
                                                                            14.7
                                                                            85
                                                                            23
                                                                            130
                                                                            63

                                                                            5.9
                                                                                                                                     927-1G

                                                                                                                                      Hi ah
                                                                                                                                     20.000
                                                                                                                                      600
                                                                                                                                      15
                                                                                                                                      33.4
                                                                                                                                      8.5
                                                                                                                                      5.1
                                                                                                                                      4000
                                                                                                                                       6
3/1/80
 13
 68
 2790
 4030
 14.3
 5.05
 235
 13.4
 85
 22
 145
 63

 6.0
            927-1H

            Hi oh
            27,500
            600
            15
            33.4
            8.5
            5.1
            4000
              9
3/2/80
 13
 69
 3030
 4005
 15.0
 5.10
 485
 20.3
 R8
 20
 125
 63   '

 8.7
           927-11

            High
           27,500
            600
            15
            33.4
            8.5
            5.1
            4000
            12
3/2/80
 21
 65
 2945
 4015
 15.3
 5.10
 555
 18.6
 91
 32

 63

 11.1
927-1K

 Hinh
27,500
 600
 15
 33.4
 8.5
 4.R
 4000
  9
3/4/f?0
 32
 59
 2245
 4050
 14.8
 4.85
 010
 12.9
 93
 26
 140
 65

 R.8
927-1L

 Hinh
20,000
 600
 15
 33.4
 8.5
 «.8
 4000
  6
3/5/80
 16
 62
 2100
 4340
 13.6
 4.80
 1010
 9.20
 90
 30
 125
 68

 6.2
            Note:  (1)  SOp removal dropped to 60? when inlet SC? concentration increased to ?ft70 ppn under replicate conditions.

-------
ro
tn
en
         100
         90 -
         80  -
      ~  70  -
      UJ
      £
      O
ca
 £S

t/1
O
a:
         40  -
         30
         20  -
                                     gP
                            °
                          0800
                                       °°
                                                                             00 O
                                                                           o    o
                                                                       AVERAGE OPERATING CONDITIONS
                                                             INLET S02
                                                             INLET LIQUOR pH
                                                             PERCENT SOLIDS
                                                             PRESSURE DROP
                                                             FLUE GAS RATE
                                                             LIQUID-TO-GAS RATIO
                                                             RESIDENCE TIME
                                        1960 - 2540 ppm
                                        5.0 - 5.2
                                        15.4
                                        8.3 inches
                                        35,000 acfm
                                        21 gal/mcf
                                        33 minutes
         HoO
         10
                              1000
                      Figure 5-1
  2000                 3000

AD I PIC ACID CONCENTRATION, ppm
4000
                                         Percent S02 Removal  vs.  Adipic Acid Concentration
                                         During Limestone  Runs  927-i/;, ID and IE
                                                                                                         5000

-------
Although S02 removal  was below 70 percent with high inlet S02 concentra-
tion, the venturi-only mode of operation with limestone/adipic acid slurry
may be viable for low-sulfur coal  applications where inlet S02 concentrations
are less than 1000 ppm.

Effect of Venturi Pressure Drop.   During Runs 927-1F, 927-1H, and 927-11, the
venturi pressure drop was varied  at 5.9, 8.7, and 11.1 inches H>>0, respectively,
For these runs, adipic acid concentration was maintained at 4000 ppm, liquid-
to-gas ratio was controlled at 27 gal/mcf, and the inlet pH was controlled at
5.1.  SOo removal was 60 percent  at 5.9 inches HoO pressure drop, and appeared
to level off at 65 to 69 percent  at 8.7 and 11.1 inches H20.


Effect of Venturi Inlet pH.   Run  927-1K was made under the same conditions as
Run 927-1H,  except for the scrubber inlet pH.  S02 removal increased signi-
ficantly from 59 percent at 2245  ppm inlet S02 concentration and at 4.85
inlet pH to  69 percent at 3030 ppm inlet S02 concentration and at 5.10 inlet
pH.  Similar sensitivity of S0? removal  to pH can be observed by comparing
Runs 927-1G  and 927-1L.
SUMMARY

Based on the test results,  the  following  conclusions  can  be made:

     •  At a liquid-to-gas  ratio  of  21  gal/mcf,  a  venturi  inlet pH  of 5.1,
        and a venturi  pressure  drop  of  8.3  inches  H20,  S02 removal  appears
        to level  off at  65  percent above  3500  ppm  adipic  acid.  (S02 removals
        greater  than 65  percent may  be  possible  at pH higher than 5.1.)

     •  Increasing the liquid-to-gas ratio  to  37 gal/mcf  (with  a somewhat
        reduced  pressure drop of  6 inches H90)  improves SOo removal  mar-
        ginally.                            L               2

     •  With low-sulfur  coals producing less than  1000  ppm inlet S0? concen-
        tration,  70 percent S02 removal should be  acnievable at 5.1 inlet
        pH,  4000  ppm adipic acid, 6  to 8  inches  H?0 pressure drop,  and 21-
        37 gal/mcf liquid-to-gas  ratio.
     e.
S02 removal  is sensitive to inlet pH (4.8 to 5.1) and adipic acid
concentration (700 to 3500 ppm),  but is insensitive to liquid-to-
gas ratio (21 to 37 gal/mcf)  and  venturi pressure drop (6 to 11
inches H20).
                                    256

-------
                                 Section  6

        LIMESTONE/ADIPIC ACID TESTING  ON THE  VENTURI/SPRAY  TOWER
                   WITH ONE TANK AND FORCED OXIDATION
Following the venturi-only  testing,  the  venturi/spray  tower  system  was modified
to allow testing in a  single-tank  forced-oxidation  mode.   Seven  runs were made,
including four runs with only  the  venturi.

Although sulfite oxidation  of  99 percent or higher  was achieved  for the  runs
with  forced oxidation, limestone blinding was  encountered  as evidenced by
poor  limestone utilization.  The long  (50 ft)  crossover line which  routed the
venturi and spray tower effluent slurries to the oxidation tank  apparently
behaved as an effective plug-flow  reactor in which  calcium sulfite  precipitated
preferentially on the  alkaline limestone particles  in  the  effluent  slurry
deficient in calcium sulfite solid crystal  seeds.
SYSTEM DESCRIPTION

Figure 6-1  is  a  schematic  flow diagram of the venturi/spray tower system using
a single tank  (D-208)  in which compressed air is injected through a  3-inch
diameter open-ended  pipe ell.   The venturi and spray tower effluent  slurries
are routed  to  the oxidation  tank  via  a 16-inch diameter crossover line  about
50 ft long. This crossover  line  is operated full  (490 gallons)  of slurry
because nearly its entire  length  is below the oxidation tank liquid  level.
The line acts  as a plug-flow reactor  as previously mentioned.  It is emphasized
that this setup  is necessitated by the limited availability of space and
is unique to the Shawnee Test Facility*

A severe cavitation  problem  in the slurry recirculation pumps during initial
startup was solved by  installing  a baffle near the pump suction nozzles and by
moving the  air injection point higher, to between the two agitator turbines.
Both turbines  propel  the slurry downward.  Figure 6-2 shows the arrangement of
the modified oxidation tank.
DISCUSSION OF  TEST RESULTS

Tables 6-1 and 6-2 summarize  the results of the single-tank forced oxidation
tests with both the venturi and the spray tower in operation, and with the venturi
alone, respectively.   The initial  test plan called for variations of the scrubber
inlet pH  and adipic acid  concentration, to observe the effects on adipic acid
consumption under forced  oxidation conditions (to compare with the results
presented in Section 4 without forced oxidation).  However, the original test
objectives were modified  in favor of a more thorough study of the limestone
blinding  phenomenon when  it was encountered.
                                       257

-------
       FLUE GAS
IVJ
£
       LIMESTONE SLURRY
       ADIPIC ACID
                                 MIST
                              ELIMINATOR
                         VENTURI
                                            FLUE GAS
                                                                                                                      MAKEUP WATER
                                               SPRAY TOWER
CROSSOVER
                                   (NOT
                                   USED)
                                              COMPRESSED
                                                  AIR
LINE (~50 FT.)
                                 EFFLUENT HOLD TANK
                                       D-101
                                                                                 \i \<
                                                                                     D
                                                                                                       CLARIFIED LIQUOR
                                                                                                       FROM SOLIDS DEWATERING SYSTEM
                                                                                                                  BLEED TO SOLIDS
                                                                                                                  DEWATERING SYSTEM
                               OXIDATION TANK
                                   D-208
                                         G-1Q5
                                                                  G-1W
                                  Figure 6-1.   Flow  Diagram for the  Venturi/Spray Tower  System
                                                  With  One Tank and Forced Oxidation

-------
                                                  NEW BAFFLE
                                                     BAFFLE SUPPORT
                      OVERHEAD VIEW OF TANK BOTTOM
TANK-MALI
  PIPE
SUPPORT
                                                    TANK WALL
                                                         NEW
                                                        BAFFLE
                     SIDE VIEW
                                                      SIDE VIEW
    Figure 6-2.   Arrangement of Modified Venturi/Spray Tower
                   Oxidation Tank (D-208)
                                259

-------
                            Table  6-1


RESULTS OF  VENTURI/SPRAY TOWER LIMESTONE/ADIPIC ACID TESTS

             WITH ONE TANK AND FORCED OXIDATION
Ma.1or Test Conditions
Fly ash loading
Gas rate, acfm 9 300°F
Venturl Hquor rate, gpm
Spray tower Hquor rate, gpm
Percent solids redrculated (controlled)
Oxidation tank residence time, m1n
Oxidation tank level, ft
Scrubber Inlet pH (controlled)
Ad1p1c add concentration, ppm
A1r rate to oxldlzer, scfm
Venturl pressure drop, Inches H20
Run-Average Results
Start-of-run date
Onstrem hours
Percent SO, removal
Inlet S02 Concentration, ppm
Ad1p1c add concentration, ppm
Ad1p1c add consumption ratio (actual/theor.)
Actual adlplc add consumption, Ibs/ton
SOj absorbed
Percent solids reclrculated
Scrubber Inlet pH
Sulflte concentration 1n Inlet liquor, ppm
SO, make-per-pass, mmole/1
Limestone utilization, %
Sulflte oxidation, %
Gypsum saturation 1n Inlet liquor, %
Centrifuge cake sol Ids, wt*
Air stolchlometry, atom 0/mole S02 abs.
M1st eliminator restriction, %
914-1A
High
35,000
600
1600
15
2.9
17
4.6
4000
200
9

3/13/80
106
91.6
19SO
4040
3.41

64.1
15.9
4.60
1250
6.1
46
98.7
145
79
1.9

914-1B
High
35,000
600.
1600
15
2.9
17
5.1
4000
2CO/300
9

3/19/80
11
(1)












9H-1C
H1ah
35,000
600
1600
15
2 A
.y
17
4.6
4000
0
9

4/7/80
47
92.6
1955
4225
1.59

43.3
14.9
4.66
862
6.1
93
32
120
65
0
3
  (1) No steady state was established due to severe limestone blinding.


                             Table  6-2



      RESULTS OF  VENTURI  LIMESTONE/ADIPIC  ACID  TESTS

              WITH  ONE TANK AND FORCED OXIDATION
Major Test Conditions
Fly ash loading
Gas rate, acfm 9 300"F
Venturi liquor rate, gpm
Percent solids redrculated (controlled)
Oxidation tank residence time, m1n
Oxidation tank level, ft
Venturl inlet Hquor pH (controlled)
Venturl Inlet Hquor limestone
stolchlometry (controlled)
Adipic add concentration, ppm
A1r rate to oxldizer, scfm
Venturl pressure drop, Inches H20
Run-Average Results
Start-of-run date
Onstream hours
Percent S02 removal
Inlet S02 concentration, ppm
Adipic add concentration, ppm
Adlpic add consumption ratio (actual/theor.)
Actual adipic acid consumption, Ibs/ton
S02 absorbed
Percent solids redrculated
Scrubber Inlet pH
Sulflte concentration in Inlet Hquor, ppm
S02 make-per-pass, mmole/1
Limestone utilization, %
Sulflte oxidation, %
Gypsum saturation in inlet Hquor, %
Centrifuge cake solids, wtt
Air stoichlometry, atom 0/mole S02 abs.
Mist eliminator restriction, *
927-1M
High
30,000
600
15
10.6
17
5.0

—
4000
300
9

3/21/80
115
71.5
2260
4170
2.19

32.0
15.0
5.05
• 75
17.1.
50
99.4
105
78
3.8
"
927-1 N
High
20,000
600
15
10.6
17
5.0

..
4000
300
91)

3/26/80
13
77.4
2030
3960
3.0

50.8
16.1
5.15
44
11.1
35
99.2
105
79
5.9
~
927-10
High
20,000
600
15
10.6
17
--

1.2
4000
300
9n

3/30/80
75
67.4
2070
4130
1.93

28.6
15.0
4.55
28
9.9
85
99.2
110
78
6.6
""
927-1 P
High
30,000
600
15
10.6
17
5.0

__
4000
0
9

4/2/80
108
69.6
2225
3960
2.26

62.5
14.9
5.07
349
16.4
54
23
125
63
0

(1) Actual pressure drop was about 7 Inches H20 because:of a problem with the adjustable plug
   mechanism and low gas flow rate.


                                   260

-------
Initial Tests.  In Run 914-1A, a  total  slurry  flow rate  of 2200  gpm  resulted
fn  Z.9 minutes residence time in  the oxidation tank (Table 6-1),  98.7  percent
sulfite oxidation in the solids,  high  inlet  liquor sulfite concentration
(1250 ppm), and poor limestone utilization of  46  percent despite  a low scrubber
inlet pH of 4.6.

To  reduce the high inlet liquor sulfite concentration, Run 914-1B was  first
run at higher pH (5.1 vs. 4.6) and  then at Increased oxidation intensity  (air
rate 300 scfm vs. 200 scfm).  However,  no indication of  increased limestone
utilization was noted and the run was  terminated.

Venturi-Only Test.  The low oxidation  tank residence time of  2.9  minutes  was
increased to 10.6 minutes during  Runs  927-1M,  927-1N, and 927-10  (Table 6-2)
by  operation of the venturi only  (600  gpm).  This necessarily raised the  S02
make-per-pass to 17.1 m-moles/liter (Run 927-1M)  which was reduced to  11.1
m-moles/liter in Run 927-1N.  The limestone  utilization  was still low  and a run
at  a controlled limestone stoichiometry of 1.2 (Run 927-10) confirmed  that lime-
stone blinding was occuring in the  crossover line because the scrubber inlet pH
of  4.55 was lower than expected.  This line  is in effect a 50 second residence time
plug-flow reactor to which is fed slurry depleted in calcium  sulfite seed crystals
and in which a favorable environment is provided  for the liquor  sulfite to
precipitate on limestone particles  before reaching the oxidation  tank.

Base Case Tests Without Forced Oxidation.  Run 927-1P was made under the  same
conditions as Run 927-1M except that the air to the oxidizer  was  shut  off to
provide a base case run without forced oxidation.   Limestone  utilization  remained
poor (54 percent) due to the combined  effect of continued high S02 make-per-pass
(16.4 m-moles/liter) and long residence time (near 50 seconds) in the  crossover
line.

Run 914-1C was made under the same  conditions  as  Run 914-1A except without
forced oxidation.  With an S02 make-per-pass of only 6.1 m-moles/liter and 13
seconds residence time in the crossover line,  combined with sufficient calcium
sulfite solid crystal seeds (32 percent oxidation), limestone utilization
improved to 93 percent.

Effect of pH and Limestone Utilization on Adi pic  Acid Consumption.   Section 4
mentioned that essentially no degradation of acipic acid occurs  at a scrubber
inlet  pH below 5.0 when oxidation is not forced.   In these tests adipic acid
degradation appeared to increase  with  forced oxidation.   In addition,  it  was
observed that poor limestone utilization increases the degradation.   These
observations are more clearly seen  in  the following table:

                                          927-1M    927-1N       927-10

    Venturi inlet pH                      5.05      5.15       4.55
    Percent limestone utilization         50         35         85
    Adipic acid consumption ratio         2.19      3.0         1.93
        (Actual/Theoretical)
    Percent unaccounted loss,of           54.3      66.7       48.2
        adipic acid
    Actual adipic acid consumption,       32.0      50.8       28.6
        Ibs/ton S02 absorbed
    Unaccounted adipic acid loss,         17.4      33.9       13.8
        Ibs/ton S02 absorbed

                                       261

-------
SUMMARY

The following is a summary of the test results and findings:

     ft  Good sulfite oxidation of 99 percent or higher was achieved in
        the solids despite poor limestone utilization.

     »  Limestone blinding occurred in the 50 ft long crossover line which
        transfers the venturi and spray tower effluent slurries to the oxidation
        tank and which behaved as an effective plug-flow reactor for calcium
        sulfite precipitation.  This peculiarity in flow configuration is
        unique to the Shawnee Test Facility.

     «  Limestone blinding caused by the long crossover line and high SO^ make-
        per-pass could not be prevented by increasing the oxidation intensity
        in the oxidation tank to reduce the sulfite concentration in the scrubber
        inlet liquor, even at SO? make-per-pass values as low as 6.1 m-moles/
        liter, and was compounded by depletion of calcium sulfite seed crystals
        in the scrubber effluent.

     •  Actual-to-theoretical  adipic acid consumption ratio and total  actual
        adipic acid requirement (Ibs per ton S02 absorbed)  increase with forced
        oxidation, increasing pH, and decreasing limestone  utilization.
                                       262

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                                 Section  7

           LIMESTONE/ADIPIC ACID TESTING ON  THE  VENTURI/SPRAY
                TOWER WITH TWO TANKS  AND FORCED  OXIDATION
Operation with two tanks  in  series,  with  forced  oxidation  in  the  first  tank
and limestone added  to  the  second  tank, has  several  advantages  over  the single-
tank operation with  forced  oxidation:

     •   Low pH (scrubber-effluent  pH)  in  the first tank  (oxidation tank)
        promotes sulfite  oxidation.

     •   The possibility of  limestone blinding by calcium sulfite  is
        decreased because fresh  limestone is added after the  oxidation
        tank.

     •   Limestone utilization  is increased with  two tanks  in  series  which
        approximate  a plug-flow  reactor for  limestone  dissolution.

     •   Extra residence time for calcium  sulfate crystallization  is  provided
        by the second tank.

     •   The second tank provides air-free suction for  the  slurry  recircu-
        lation and bleed  pumps,  thus avoiding pump cavitation.

Earlier test results from the  TCA  system  with limestone/adipic  acid  and forced
oxidation have shown two-tank  operation to be superior to  the single-tank
mode (Reference 3).  Eight  runs  (Runs 916-1A through 916-1H)  were made  to
confirm this conclusion on  the venturi/spray tower system  using two  tanks  in
series. A schematic flow diagram  is shown in Figure 7-1.   Air  is injected
into the first tank  (D-208)  while  limestone  and  adipic acid are added to the
second  tank (D-101). The detailed arrangement of the  oxidation tank (8 ft
diameter) is shown in Figure 6-2.
DISCUSSION  OF  TEST  RESULTS

Table 7-1 summarizes  the  results  of the eight runs made with two  tanks  in  series,
including one  run  (Run  916-1H)  without forced oxidation.   In general,  good
S02 removal  was  achieved  with  excellent oxidation of the solids for all  the
forced oxidation tests.   However, as in the tests with forced oxidation
using a single tank (Section 6),  calcium sulfite blinding of limestone  in
the crossover  line  continued to reduce the limestone utilization  below
the level normally  expected with  two-tank operation.   This remained true
despite the efforts to  increase limestone utilization by either increasing the
oxidation intensity or  lowering the S02 make-per-pass.
                                     263

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                                                FLUE GAS
     FLUE GAS
cn
    LIMESTONE SLURRY

    ADIPICACID
                                REHEAT
COMPRESSED
   AIR
                            G-104    EFFLUENT HOLD TANK
                            ~D-101
                                                                                                               MAKEUP WATER
                                                                                                            CLARIFIED LIQUOR
                                                                                                            FROM SOLIDS
                                                                                                            DEWATERING SYSTEM
                                                                                                                    BLEED TO
                                                                                                                     SOLIDS
                                                                                                                   DEWATERING
                                                                                                                  	SYSTEM
                                  Figure 7-1.   Flo» Diagram for  the Venturi/Spray  Tower System
                                                 Wi Ui "iwo  Tanks and  FoT^d- Oxidation

-------
                                                              Table  7-1
                                RESULTS OF VENTURI/SPRAY TOWER  LIMESTONE/ADIPIC ACID TESTS
                                              WITH  TWO TANKS  AND  FORCED  OXIDATION
Major Test Conditions
Fly ash loading
Flue gas rate, acfm 1? 300°F
Venturi liquor rate, gpm
Spray tower liquor rate, gpm
Percent solids reclrculated (controlled)
EHT res. time (mini/tank level (ft)
Ox1
—
7.5-7.7
916-10
High
30,000
600
1200
15
11.1/8.5
3.8/18
5.1
1500
1.5

6

5/6/80
163
92.4
2220
1490
—
--
15.0
5.12
5.03
72
99.8
105
81
1E9l>
84(3)
—
7.3
916-1E
High
20,000
600
1600
15
9.1/8.5
3.1/18
5.1
1500
1.5

7

5/13/80
145
98.0
1880
1540
4.89
8.91
14.Q
5.13
5.00
86
P9.5
105
60
90m
88(3)
—
3.6
916-1F
High
30,000
600
1200
15
11.1/8.5
3.8/18
5.4
1500
1.5

6

5/19/80
71
89.2
2260
1510
2.30
7.75
15.9
5.14
5.06
46
99.4
145
583
#«

7.1
916-16
High
30,000
600
1200
15
11.1/8.5
3.8/18
5.4
1500
2.5

6

5/22/80
61
93.7
2150
1550
3.32
8.76
15.6
5.33
5.24
61
99.6
120
33
?46
85(3)

7.1
916-1H
High
30,000
600
1200
15
11.1/8.5
3.8/1R
5.1
1500
0

6

5/24/80
P4
85.5
2500
1440
2.03
11.4
15.6
5.12
4.77
96
50.4
120
317
°59»>
1
7.6
(1)  Venturi operated with plug wide open for all  rufis  except for Run 916-1A where pressure drop was
    controlled at 9 inches H20.

(2)  System operated with clarifier only.

(3)  Drun filter used in place of centrifuge.

-------
Forced Oxidation Testing.   During the testing covered by Runs 916-1A through
916-1G, several  measures  were taken to eliminate or minimize the effect of the
crossover line.   Operating parameters explored included:

     •  Liquid-to-gas ratios in the spray tower of 17.8 to 100 gal/mcf

     «  S02 make-per-pass of 3.6 to 12.0 m-moles/liter

     •  Adi pic acid concentrations of 1490-4015 ppm

     e  Scrubber inlet pH of 4.77 to 5.33

     •  Air stoichiometry to the oxidizer of 1.5 to 2.5 atoms 0/mole S02
        absorbed

However, the overriding tendency of the crossover line to act as a plug-
flow reactor, as described in Section 6, could not be eliminated.

Base Case Test Without Forced Oxidation.  Run 916-1H was made under the same
conditions as Run 916-ID  except that the air to the oxidizer was turned off.
Significantly, the limestone utilization improved to 96 percent because suffi-
cient calcium sulfite solid seeds were available (50.4 percent oxidation)  and
blinding of limestone by  calcium sulfite in  the crossover line was eliminated.

SUMMARY

The following is a summary of the test results:

     •  Good S02 removal  and excellent sulfite oxidation (99.4 to  99.8  percent)
        were achieved with the two-tank forced oxidation system.

     •  Limestone utilization for the two-tank operation was higher than for
        single-tank operation (Section 6)  but below that expected  with  two-tank
        operation without limestone blinding.

     •  As in the single-tank operation with forced oxidation (Section  6),
        limestone blinding caused by the crossover line and  high S02 make-
        per-pass cannot be eliminated by increasing the oxidation  intensity
        to reduce sulfite  concentration in the scrubber inlet liquor.

     •  Reducing the S02 make-per-pass (Run  916-1E),  and hence the scrubber
        effluent sulfite concentration,  improved limestone utilization  but
        not to the expected 1evel.
                                       266

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                                Section 8

             BLEED STREAM OXIDATION OF LIMESTONE/ADIPIC  ACID
               SLURRY FROM THE VENTURI/SPRAY  TOWER  SYSTEM
In April 1979, prior to this  reporting  period,  five  bleed  stream  oxidation
tests were made on the venturi/spray  tower system  using  limestone slurry with
1500 ppm of adipic acid (Reference  3).   At that time,  good sulfite oxidation
of 99 percent was achieved when  the slurry pH  in the oxidation  tank was kept
below about 6.0 by recycling  60  gpm of  oxidation tank  slurry  back to  the ef-
fluent  hold tank.  Satisfactory  oxidation  (95  percent) was also obtained
without the recycle, but at the  high  oxidation  tank  residence time of about
7.5 hours for the bleed stream.

Recent  tests with adipic acid additive  have demonstrated several  advantages of
operating at low pH and high  adipic acid concentration (see Section 4).  There-
fore, three tests (Runs 915-1A,  915-1B,  and 915-1C)  were conducted in April
1980 to see if operating at reduced pH  was conducive to  bleed stream  oxidation.
The flow diagram of the bleed stream  oxidation  tests on  the venturi/spray tower
system  is shown in Figure 8-1.   The same oxidation tank  used  in one-tank and
two-tank in-loop forced oxidation  (Sections 6  and  7) was used in  these three
tests.  The detailed arrangement of the oxidation  tank is  shown in Figure 6-2.
DISCUSSION  OF  TEST  RESULTS

The'results of bleed stream oxidation tests at low pH are given  in  Table 8-1.
All  tests achieved  better than  95  percent S02 removal at 4.8  to  5.1 scrubber
inlet  pH and  about 4000 ppm adipic  acid.  Average limestone  utilizations were
88 to 91 percent.

Good sulfite oxidation of 98 percent was achieved only in Run 915-1C when the
scrubber inlet pH was controlled at  4.8 with an air stoichiometry of 1.80 atoms
oxygen/mole SO? absorbed.  Oxidation was only about 70 percent at 5.0 scrubber
inlet pH and 1.55 air stoichiometry  (Run 915-1A), or at 5.1 scrubber inlet. pH
and 2.10 air stoichiometry (Run 915-1B).

The oxidation  tank  pH was 5.4,  5.7,  and 4.8 for Runs 915-1A,  915-1B, and 915-.C,
respectively,  as compared with  5.5 to 5.6 for runs made earlier in  April 1979 when
good oxidation was  achieved at  1.50  to 1.85 air stoichiometry.  The lower oxida-
tion efficiency for the recent  tests may be attributed to the poor oxidizer
arrangement shown in Figure 6-2.

As has been observed previously, adipic acid degradation increased with pH
during these runs.   For Runs 915-1C, 915-1A, and 915-1B, under similar lime-
stone utilizations, the actual-to-theoretical adipic acid consumption ratios
were 1.26,  3.33, and 5.20, respectively, when the scrubber inlet pH increased
from 4.8 to 5.0 and to 5.1, and the  oxidation tank pH increased concurrently
from 4.8 to 5.4 and to 5.7.  Actual  adipic acid consumption increased from 15,4
to 40.1 and to 44.5 Ibs/ton S02 absorbed, respectively.


                                       267

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    REHEAT
G.1M    EFFLUENT HOLD TANK

              D-101
                                                                                   MAKEUP WATER
                                                                               CLARIFIED LIQUOR
                                                                               FROM. SOLIDS
                                                                               DEWATERING SYSTEM
                                                                                       BLEED TO
                                                                                        SOLIDS
                                                                                      DEWATERING
                                                                                       SYSTEM
G-105
   Figure 8-1.   Flow Diagram for Bleed Stream  Oxidation  in the
                  Ventur-1/Spray Tower System

-------
                                                      Table 8-1
                            RESULTS OF VENTURI/SPRAY TOWER  LIMESTONE/ADIPIC ACID TESTS

                                            WITH  BLEED  STREAM OXIDATION
fro
cr>
(£>
Major Test Conditions
Fly ash loading
Flue gas rate, acfm P 300°F
Venturi liquor rate, gpm
Spray tower liquor rate, gpm
Percent solids recirculated (controlled)
EHT Res. time (min)/tank level (ft)
Oxid. Tk. Res. time (mini/tank level (ft)
Scrubber inlet pH (controlled)
Adipic acid concentration, ppm
Air rate to oxidizer, scfm
Venturi pressure drop, inches 1^0
Run-Average Results
Start-of-run date
Onstream hours
Percent S02 removal
Inlet SOg concentration, ppm
Adipic acid concentration, ppm
Adipic acid consumption ratio, (actual/theor.)
Actual adipic acid consumption, Ibs/ton Sf^ absorbed
Percent solids recirculated
Scrubber inlet pH
Oxidation tank pH
Limestone utilization, %
Sulfite oxidation in oxidation tank, %
Sulfite oxidation in scrubber inlet, %
Gypsum sat'n. in oxidation tank, %
Gypsum sat'n. in scrubber inlet, %
Oxidation tank liquor SO? concentration, ppm
Air stoich., Ib atoms 0/1 h mole S02 absorbed
Centrifuge cake solids, wti
Mist eliminator restriction, %
915-1A
High
35,000
600
1600
15
9.1/8.5
-m
5.1
4000
200
9

4/10/80
98
97.6
2340
38^0
3.33
40.1
15.2
4.99
5.40
91
69
26
105
120
115
1.55
70

915-1B
Hiah
35,000
600
1600
15
9.1/8.5
-/17
5.1
4000
300
9

4/14/80
24
98.0
2550
4045
5.20
44.5
15.5
5.09
5.70
90
73
25
105
115
95
2.10
79

91 5- 1C
High
35,000
600
1600
15
9.1/8.5
-/17
4.8
4000
200
9

4/15/80
127
96.0
2030
4140
1.26
15.4
15.6
4.82
4.80
88
98
54
100
105
140
1.80
79
3

-------
Previous Shawnee data indicated that the dewaten'ng properties of slurries
from bleed stream oxidation are better than those of unoxidized slurries
but inferior to those from in-loop forced oxidation.  For Run 915-1C, with
98 percent sulfite oxidation and 4140 ppm adipic acid, the initial settling
rate of solids averaged only 0.3 cm/min, somewhat better than the 0.2 cm/min
settling rate for unoxidized slurry (see Section 10).   For the bleed stream
oxidation runs made in April  1979, the average settling rate was much higher
at 0.8 cm/min for slurries with good oxidation (95 percent or higher) and
with lower 1500 ppm adipic acid concentration.  These  values for bleed stream
oxidation are in the lower range of 0.3 to 1.6 cm/min  reported in Table 10-1
for all the oxidized limestone slurry with adipic acid.
SUMMARY

At a scrubber inlet pH of 4.8  and  about  4000  ppm adipic  acid concentration,
98 percent oxidation of sulfite  was  achieved  in  the  bleed stream oxidation tank
(4.8 pH) with an air stoichiometry of  1.8  atoms  oxygen/mole SO? absorbed.
The S02 removal  was 96 percent at  2030 ppm inlet S02 concentration and the
limestone utilization was 88 percent.  The actual-to-theoretical  adipic acid
consumption ratio was 1.26 and the actual  adipic acid consumption was  15.4
Ibs/ton S02 absorbed (8.7 Ibs/ton  limestone fed).
                                      270

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                                Section 9

                  LIMESTONE BLINDING  BY CALCIUM  SULFITE
Blinding of limestone as evidenced  by  low  limestone  utilization has been
encountered during limestone  tests  with  and  without  adipic acid enhancement.

The limestone blinding  is most common  under  in-loop  forced oxidation condi-
tions, where the recirculated slurry is  deficient  in solid calcium sulfite
crystal seeds and the calcium sulfite  in the liquor  preferentially preci-
pitates on, and blinds, the alkaline limestone  particles.  This section describes
system behavior during  limestone  blinding, the  conditions leading to it, and
recommended solutions for eliminating  or avoiding  limestone  blinding.
SYSTEM BEHAVIOR  DURING  LIMESTONE  BLINDING

Limestone  blinding  in a scrubber  system is  normally characterized by  the
following  phenomena:

     •  Severe drop in  slurry  pH

     •  Very  insensitive pH  response  to limestone addition  at  low pH

     •  Poor  limestone  utilization

     •  High  sulfite concentration  in the  liquor


The first  indication of limestone blinding  is a  precipitous drop in the pH
of the recirculating slurry  for no  apparent reason.  In  order  to control  system
pH, the operator normally begins  to increase the limestone  feed rate,  leading
to poor limestone utilization.  Limestone  utilization as low as 20 to  25
percent has been observed at Shawnee.  While the pH response to the limestone
feed rate  is  normally more sensitive  at a  low pH range of 4.5  to 5.5  (less
limestone  buffer) than  at a  high  pH range  of 5.5 to 6.5  (more  limestone
buffer), the  response is typically  sluggish even at low  pH  when limestone
blinding occurs.
CONDITIONS  LEADING  TO  LIMESTONE  BLINDING

The necessary conditions  for blinding to occur are:

     •  Slurry solids  deficient  in  calcium sulfite crystal  seeds

     •  High  sulfite concentration  and/or supersaturation in the  slurry
        liquid
                                       271

-------
The slurry solids deficient in calcium sulfite crystal  seeds (i.e., high
gypsum content) can be a result of forced oxidation or high natural oxidation,
Experience at Shawnee indicates that limestone blinding does not occur at
sulfite oxidation levels in solids below approximately 85 percent under most
of the operating conditions.

When the slurry solids contain an insufficient amount of calcium sulfite
crystals, the saturated sulfite in the liquor tends to precipitate pre-
ferentially on alkaline solid particles such as limestone, because the
solubility of calcium sulfite is a strong function of pH and decreases with
increasing pH.  Thus, even if the bulk liquor is not supersaturated with
sulfite, as may be the case with low bulk liquor pH, supersaturation and
precipitation could occur in the high pH region in the vicinity of the lime-
stone particles, causing blinding.

High sulfite concentration or supersaturation can be caused by:

     «  Insufficient oxidation intensity (affecting both scrubber inlet and
        outlet)

     •  High S02 make-per-pass (affecting scrubber outlet)

The use of additives, such as adipic acid,  enhances the S02 removal and
increases the S02 make-per-pass, thus increasing the potential  for limestone
blinding.
RECOMMENDED SOLUTIONS

Operating Considerations.   Limestone blinding by calcium sulfite is the result
of calcium sulfite-deficient slurry solids  (high gypsum content) and high cal-
cium sulfite supersaturation (or high sulfite concentration)  in the liquor.  The
latter can be caused by insufficient oxidation intensity, high S02 make-per-pass
or both.

Therefore, any measures that can reduce these effects will  reduce the chance of
limestone blinding.   Better oxidation can be obtained by:

     o  Increasing the air stoichiometry

     »  Increasing the oxidation tank level  to provide a longer air bubble
        residence time

     «  Increasing the oxidation tank agitation

This would reduce the sulfite saturation and concentration  at the scrubber
inlet.

The level of sulfite in the scrubber effluent liquor can be reduced by reducing
the inlet liquor sulfite as above or by reducing the S02 make-per-pass.
Lower S02 make-per-pass can be obtained by  lowering the flue  gas throughput,
increasing the slurry flow rate, or both.

                                       272

-------
Design  Considerations.   If an  in-loop forced oxdiation system with a  single
tank is desired,  then  provision should be made:

     •   To provide an  adequate oxidation intensity to minimize sulfite
        saturation at  the scrubber inlet

     •   To reduce S02  make-per-pass (outlet sulfite concentration)

A better solution appears to be the use of two tanks in series,  which provide
several advantages over the single-tank mode listed in Section 7.

Limestone blinding in  the long scrubber effluent line (Sections 6  and 7),  which
acts as a plug-flow reactor, is unique at Shawnee.  In full-scale  design,  the
scrubber effluent piping should be as short as possible to minimize the poten-
tial for limestone blinding.
                                       273

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                                Section 10

                       DEWATERING CHARACTERISTICS OF
               ADIPIC ACID-ENHANCED LIME/LIMESTONE SLURRIES
Cylinder settling tests and vacuum funnel  filtration tests are routinely
conducted in the Shawnee Laboratory to monitor the settling and dewatering
characteristics of slurry solids.

In the previous reports (References 2 and 3), a comparison of the results
of these monitoring tests from July 1978 through October 1979 was presented
for lime and limestone slurry with and without adipic acid addition.  It
was found that adipic acid has an insignificant effect on the quality of
solids (settling rate and filterability),  except that the settling rate of
oxidized limestone slurry may be retarded.

Table 10-1 has been updated to include additional  data, obtained from October
1979 through May 1980, for limestone slurry with adipic acid addition both
with and without forced oxidation.

The updated data show a higher average initial  settling rate of 0.9 cm/min
(0.3 to 1.6 cm/min range) for oxidized limestone slurry with adipic acid,
compared to the 0.6 cm/min (0.3 to 0.9 cm/min range) previously reported for
the same type of slurry (Reference 3).   The average initial  settling rate for
oxidized limestone slurry without adipic acid remains the same at 1.1 cm/min.

The settling rate of unoxidized limestone  slurry again shows essentially
no effect from adipic acid.  The average settling  rate is 0.2 cm/min with
or without adipic acid.
                                       274

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                                                 Table  10-1

                            COMPARISON OF  SHAWNEE WASTE SLURRY  DEWATERING
                       CHARACTERISTICS WITH AND WITHOUT ADIPIC ACID ADDITION






ro
-j
en




Alkali
Limestone' '
Limestone. .
Limestone131
Limestone


Lime
Lime
Lime
Lime

Fly Ash .
Loading11'
High
High
High
High


High
Hioh
High
Hi(jh

Forced
Oxidation
Yes
Yes
No
No


Yes
Yes
No
No

Adi Die
Acid(z)
Yes
No
Yes
No


Yes
No
Yes
No
Initial
Solids
Cone., wt %
IF
IS
15
15


8
8
8
ft
Initial
Rate,
Avg.
0.9
1.1
0.2
0.2


1.7
_
1.5
1.5
Settlino
cm/mi n.
Ranne
0.3-1.6
n.fi-1.4
0.1-0.4
0.1-0.5


1.5-1.9
_
1.2-1.9
O.P-2.2
Ultimate
Solids
Avg.
70
73
50
51


55
_
51
49
Settled
, wt %
Ranpe
57-P3
62-flfi
37-69
41-67


50-60
_
44-63
43-57
Funnel Test Cake
Solids,
Avg.
70
74
56
57


61
-
62
56
wt %
Range
59-77
65-8P
48-73
48-66


54-69
-
48-73
50-62
(1)  Slurries with hioh fly ash loadinn contain about 40 percent fly ash in solids.
(2)  Adipic acid concentration range is 300 to 4500 ppro.
(3)  Data have been updated to include test results from October 1979 throunh May

-------
                                Section  11
                     ECONOMICS  OF  ADIPIC  ACID-ENHANCED
                            LIMESTONE  SCRUBBING
The economics of adipic  acid-enhanced  limestone scrubbing has been projected
for forced-oxidation systems  designed  to  achieve an  average of 90 percent
S02 removal  from high sulfur  flue  gas.  The  results  indicate that, for the
cases studied, both capital and  operating costs are  approximately 4 to 6
percent lower for adipic acid-enhanced limestone systems than for a lime-
stone system without additive.   The  major savings are in the reduced lime-
stone requirement and the associated grinding  equipment.  Additional  1 to 2
percent savings in operating  cost  result  from  the reduced quantity of waste
solids that  need to be disposed  of in  the adipic acid-enhanced limestone system.

The operating conditions for  four  study cases,  including a limestone case
with MgO additive, were  prepared by  Bechtel  and are  presented in  Table 11-1.
The capital  investment and revenue requirement were  calculated by the
Economics Evaluation Section  of  TVA's  Energy Design  and Operations Branch
using a TVA/Bechtel  Design-Economics Computer  Program (Reference  8).   The
results are  listed in Table 11-2.  The evaluations are based on a 500-MW
scrubbing facility incorporating forced oxidation and operating on flue gas
from a boiler burning 4  wt %  sulfur  coal.  The capital  investment and revenue
requirement  in Table 11-2 include  the  dewatering equipment (thickener and filter)
but exclude  the waste sludge  (filter cake) disposal  area.

The cases evaluated are:

        Case 1 - A limestone  base  case without additive operated  at rela-
                 tively  high  limestone stoichiometry and liquid-to-gas
                 ratio to achieve  90 percent S02 removal.   It should be
                 noted that long-term  reliability with this mode  of opera-
                 tion has not been demonstrated at Shawnee.

        Case 2 - A limestone  case  with MgO addition.  Oxidation of the
                 scrubber bleed  stream was chosen because in-loop
                 oxidation is incompatible with magnesium-enhanced
                 scrubbing.   As  in Case 1, long-term reliability  has not
                 been demonstrated at  Shawnee  for this mode of operation.

        Case 3 - A limestone  case  with adipic  acid addition operated at
                 high pH.   Although  only  800 ppm of  adipic acid is required
                 to obtain 90 percent  S02 removal, degradation of adipic
                 acid at high pH requires about five times the theoretical
                 adipic  acid  addition  rate.

        Case 4 - A limestone  case  with adipic  acid addition operated at low
                 pH.   For this case, 2000 ppm  adipic acid is required.
                 However,  the low  pH operation requires only 1.4  times the
                 theoretical  adipic  acid  addition rate and 1.05 limestone
                 stoichiometry.

                                       276

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                                 Table 11-1

              CONDITIONS FOR ECONOMIC ANALYSIS OF ADIPIC ACID-
             ENHANCED LIMESTONE SCRUBBING WITH FORCED  OXIDATION
Capacity:
Coal:
Scrubber:

SO* Removal Efficiency:
Superficial Gas Velocity:
Number of Trains:
Solids Dewatering:

Onstream Factor:
Effluent Hold Tank Residence Time;
Oxidation Tank Residence Time:
Oxidation Tank Level:
Air Sparger Pressure Drop:
Oxidation Tank Agitator Hp:
Solid Sulfite Oxidation:
Air Stoichiometry:
Number of Tanks:
                             500 MW
                             4 wt% sulfur
                             TCA with 3 beds, 4 grids, and 5 inches
                             of static height of spheres per bed
                             90%
                             12.5 ft/sec
                             5, including 1 spare train
                             To 80 wt% solids by thickener and rotary
                             drum vacuum filter
                             5500 hours/year
                             5 minutes
                             5 minutes
                             18 ft
                             5 psi
                             0.002 Brake Hp/gal
                             99%
                             1.7 Ib-atpms 0/1b mole S02 absorbed
                             2 (effluent hold tank and oxidation tank)
Case No.
Alkali-
Additive

Additive Concentration, ppm
Additive Rate, Ib/hr
L/G, gal/mcf
Limestone Stoichiometry,
moles Ca/mole SOo absorbed
TCA Inlet pH '
Mode of Oxidation(d)

1
Limestone
-

_
-
58

1.52
5.8
in loop

2
Limestone
MgO

5500 (a)
104
50

1.20
5.4
bleed
stream
3
Limestone
Adi pic
Acid
800 fhl
83.3(b)
50

1.20
5.6
in loop

4
Limestone
Adi pi c '•
Acid
2000,
53.6^ i
50

1.05
4.8
in loop

Notes:
(a)
(b)
(c)
(d)
Effective Mg++ concentration.
Five times theoretical consumption.
1.4 times theoretical consumption.
In-loop oxidation with two tanks  uses  an  oxidation tank
followed in-series by an effluent hold tank  where alkali
is added.  Bleed stream oxidation uses one effluent hold
tank in the scrubber loop and one bleed stream tank where
air is injected.
                             277

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As shown in Table 11-2,  both the total  capital  investment and the first
year revenue requirement are the lowest for adipic acid-enhanced limestone
scrubbing at low pH (Case 4).  The total  capital  investment is reduced by
4.8 percent and the first year revenue  requirement reduced by 5.8 percent
for the limestone/adipic acid/low pH case (Case 4) compared with the con-
ventional limestone case (Case 1).  The revenue requirement includes 14.7
percent annual capital  charge.

Total capital investment and operating  cost for adipic acid-enhanced lime-
stone at high pH (Case  3) are higher than those for limestone/adipic acid
at low pH (Case 4), but are still lower than those for the conventional
limestone (Case 1) or the 1 imestone/MgO case (Case 2).  Total capital
investment is lower by  3.9 percent and  the first year revenue requirement
is lower by 4.0 percent for Case 3, compared with Case 1.

Note that the capital  investment and revenue requirements shown in Table 11-2
are significantly different from those  presented by TVA in an earlier session.
This is due to differences in process equipment and operating parameters
itemized in Table 11-3.   The most significant factors are coal sulfur content,
scrubber type, superficial gas velocity,  L/G, hold tank residence time,  and
landfill investment (not included in Bechtel comparison).  The operating
parameters in Table 11-1 were selected  to represent conditions which have been
tested at Shawnee.  If  the basic design parameters for the comparison in
Table 11-1 were adjusted to be the same as those used in the earlier TVA
comparison, the same relative results (i.e., limestone scrubbing with
adipic acid addition is slightly more economical  than standard limestone
scrubbing) would be obtained.

Table 11-4 illustrates  the additional savings that result from adipic
acid addition.  Because of the lower pH operation, and thus lower
limestone consumption,  the amount of waste solids produced is lower for
limestone/adipic acid cases (Cases 3 and  4) than for a limestone case
(Case 1).  Assuming a landfill disposal cost of $10/dry ton, including
14.7 percent annual capital  charge, the first year revenue requirements
for the sludge disposal  area are 0.97,  0.83, and 0.77 mills/kWh for
Cases 1, 3, and 4, respectively.  Thus, the total first year revenue
requirement is 9.34 mills/kWh for Case  4  compared with 10.06 mills/kWh
for Case 1.  This is a  reduction of 7.2 percent,  compared with 5.8 percent
when the sludge disposal cost is not included.

It should be noted that the differences in total  capital investments and
operating costs amoung  these cases are  small.  Furthermore, the cost
figures are not meant to be accurate or representative of actual scenarios.
The principal conclusion from these evaluations is that adipic acid addition
does not increase costs but decreases them slightly on the same comparison
basis.
                                      278

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                               Table 11-2

              RESULTS OF ECONOMIC ANALYSIS OF ADIPIC ACID-
           ENHANCED LIMESTONE SCRUBBING WITH FORCED OXIDATION
Case No. Additive
1
2 MgO
3 Adipic Acid
4 Adipic Acid
Total Capital
Additive Investment^'
Cone., ppm $MM(1982)
87.40
5500 85.26
800 83.97
2000 83.22
$7kW
174.8
170.5
167.9
166.4
First Year
Revenue , w ,
Requirement(bMc)
$MM(1984) r
25.01
24.15
24.01
23.56
1il 1 s/kWh
9.09
8.78
8.73
8.57
Notes:  (a)  Effective Mg+  concentration.
       (b)  Does not include waste sludge disposal area.
       (c)  Includes 14.7% annual capital charge.

Raw Material Costs (1984):  Limestone   - $8.5/ton
                           MgO         - $460/ton
                           Adipic Acid - $1200/ton
                               Table 11-3

                      LIMESTONE PROCESS COMPARISON

Item
Type scrubber
Superficial gas velocity
fc sulfur in coal (as fired)
Effluent hold tank residence time
Oxidation tank residence time
Air stoichiometry
Landfill investment
Adipic acid
L/C
Limestone stoichiometry
Adipic acid consumption ratio ( actual /theor.)
Bechtel
(Case 3)
TCA
12.5 ft/ sec
4.0
5 min
5 min
1.7
Not included
800 ppm
50
1.2
5

TVA
Spray tower
10 ft/ sec
3.36
12 min
5 min
2.5
Included
1000 ppm
80
1.2
3
                                       279

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                            Table  11-4

                      REVENUE  REQUIREMENT IN
                       SLUDGE  DISPOSAL  AREA
Filter Cake,
Case No. dry tons/hr
1 48.7
2 41.6
3 41.6
4 38.3
First Year Revenue
Total Excluding. .
Sludge Disposal ID)
9.09
8.78
8.73
8.57
Rquirement,
Sludge
Disposal10'
0.97
0.83
0.83
0.77
Mills/kWh(a)
Total
10.06
9.61
9.56
9.34
Notes: (a)   Includes 14.7%  annual  capital  charge.
            Costs are based on  1984  dollars.
       (b)   From Table 11-2.
       (c)   Assumes $10/dry ton,  including 14.7% annual  capital  charge.
                                   280

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                               Section 12

                         SUMMARY OF CURRENT WORK
Important test results of adipic acid-enhanced .limestone scrubbing (with
high fly ash loading) on the venturi/spray tower system from October 1979
through May 1980 are summarized below.  The summary of previous work
through October 1979 has been presented in Section 2.

    •  Factorial tests with spray tower only (venturi plug wide open
       with 125 gpm slurry flow) showed that, within the operating
       ranges of 15 to 75 gal/mcf spray tower liquid-to-gas ratio, 4.6
       to 5.9 scrubber inlet pH, and 600 to 2400 ppm adipic acid con-
       centration, each 0.4 unit drop in the scrubber inlet pH requires
       a 700 ppm increase in adipic acid concentration to achieve a
       similar percent S02 removal.

    •  Apparent degradation of adipic acid is quenched at low pH.*  Without
       forced oxidation, essentially no degradation occurs at a scrubber
       inlet pH below about 5.0.  Both forced oxidation and high limestone
       stoichiometry (due to limestone blinding at low pH conditions) con-
       tribute to higher adipic acid degradation.

    •  Operating a scrubber at low pH and high adipic acid concentration can
       actually result in lower total adipic acid consumption than operation
       at a high pH and low concentration for the same S02 removal.

    •  The optimum scrubber inlet pH appears to be 5.0 to 5.1 with respect
       to adipic acid consumption, limestone utilization, and the sensitivity
       of S02 removal to pH and inlet S02 concentration.

    •  Operation with the venturi alone (slurry flow to the spray tower
       turned off) without forced oxidation indicated that the SO? removal
       levels off at a maximum value of about 65 percent at 2000 to 3000
       ppm inlet SO? concentration, with 3500 to 4500 ppm adipic acid, 21
       gal/mcf liquid-to-gas ratio, 5.1 venturi inlet pH, and 8.3 inches
       HoO venturi pressure drop.  This mode of operation could, however, be
       attractive for low-sulfur coal having less than 1000 ppm inlet S02
       concentration where only 70 percent S02 removal is required.

    •  In an in-loop forced oxidation system, or in a system with high natural
       oxidation, blinding of alkaline limestone particles by calcium sulfite
       could occur because of the deficiency in calcium sulfite seed crystals.
       Operation with two tanks, with forced oxidation in the first tank and
       limestone added to the second tank, minimizes the potential for lime-
       stone blinding.
*  Recent laboratory test results at the University of Texas at Austin
   (Reference 9) have shown that the adipic acid degradation decreases in
   the presence of Mn ion, and also decreases with pH when Mn is present.
   The IERL-RTP pilot plant test results (Reference 10) have identified Mn
   and Fe ions as possible inhibitors of adipic acid degradation.

                                      281

-------
«  A long scrubber slurry-filled effluent pipeline (a flow configuration
   which exists at Shawnee on the venturi/spray tower system due to
   system constraints)  is detrimental  in that it could act as an effect
   tive plug-flow reactor for calcium sulfite precipitation and increase
   the potential  for limestone blinding.  Limestone blinding in this manner
   cannot be totally eliminated by increasing the oxidation intensity
   because calcium sulfite precipitates before being oxidized.

•  Additional  data showed that adipic  acid only slightly reduces the
   settling rate of oxidized limestone slurry, to 0.9 cm/min (vs.  0.6
   cm/min previously reported) from 1.1 cm/min for oxidized limestone
   slurry without adipic acid.

•  Economic analyses for a TCA system  with 90 percent S02 removal  from
   4 percent sulfur coal  show that both capital  and operating costs,
   excluding the waste  solids disposal  area, are approximately 4 to 6
   percent lower for limestone scrubbing systems with 800 to 2000  ppm
   adipic acid than for a limestone system without additive.  Additional
   savings for limestone systems with  adipic acid can be realized  in the
   waste solids disposal  area because  of lower solids production rate.
                                  282

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                               Section 13

                        FUTURE SHAUNEE TEST PLAN
The test program for the Shawnee Test Facility, as  presently conceived for
the remainder of 1980 and 1981, is  presented below.  The major effort will
still  be placed on the adipic  acid-enhanced limestone  scrubbing.

In late-May and the first-half of June  1980, Train  100 was converted from a
venturi followed by a spray  tower to a  spray tower-only system.   In addition,
the spray tower piping and the internal  headers were modified in  August 1980
to increase the maximum slurry flow rate from  1600  gpm to 2400 gpm.  The
following test activities with the  spray tower only are either in progress,
planned, or suggested:

     t Factorial tests with limestone  slurry  with  or without forced oxida-
       tion, and with or without adipic acid  addition, to expand the existing
       data base and computer models for predicting $62 removal.

     • Long-term (500 hours)  demonstration tests with the spray  tower only
       using limestone/adipic acid slurry with and without forced oxidation.

     • Tests to develop design criteria for the spray tower internals.

     • Tests with packings  having  low  pressure drop,  high efficiency, and
       low plugging and scaling potential, such as Glitsch Grid  packing.

     t Tests with other organic acid additives such as dibasic acid, which
       is a byproduct of adipic acid manufacture consisting primarily of
       adipic, glutaric, and  succinic  acids.

     • Tests with low S02 during the Boiler No. 10 baghouse acceptance
       testing.

     • Integrated power plant water management testing, such as  water reuse
       and additive recovery.

     • Testing with other alkalis, such as water treatment sludge, partially
       calcined limestone,  and hydrated dolomitic  lime.

The TCA system  (Train 200) was restored from a DOWA basic aluminum sulfate
process operating configuration in  late-June 1980.  The following activities
are either proceeding, planned, or  suggested:

     t Simulation of the two  full-scale TCA units  operating with adipic
       acid-enhanced limestone at  the  Southwest Station of the Springfield
       City Utilities at Springfield,  Missouri, as part of the EPA full-
       scale adipic acid demonstration program.

     • Automatic limestone  feed control  testing.

     • Testing with sodium  thiosulfate as an  oxidation inhibitor.

                                     283

-------
     •  Tests with Glitsch Grid packing in  lieu  of spheres.
     «  Tests with other organic acid  additives,  such as dibasic acid.
     «  Development of a magnesium or  calcium adipate clear  liquor
        scrubbing process.
     »  Development of other forced oxidation methods.
     9  Tests with low S02 during the  Boiler  No.  10  baghouse acceptance
        testing.
     •  Investigation of the effects of limestone type  and grind on SO?
        removal and limestone utilization.
Some of the tests listed above are interchangeable between Train 100 and
Train 200.
                                     284

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                                Section 14

                                REFERENCES
 1.  Borgwardt, R. H., "Significant EPA/IERL-RTP Pilot Plant Results," in
    Proceedings:  Industry Briefing on EPA Lime/Limestone Wet Scrubbing
    Test Programs (August 1978), EPA-600/7-79-092 (NTIS PB 296517),
    March 1979 (pp.1-9).

 2.  Head, H.N., et al., "Recent Results from EPA's Lime/Limestone Scrubbing
    Programs - Adipic Acid as a Scrubber Additive," in Proceedings: Symposium
    on Flue Gas Desulfurization - Las Vegas, Nevada, March 1979; Volume I,
    EPA-600/7-79-167a (NTIS PB 80-133168), July 1979 (pp. 342-385).

 3.  Burbank, D.A., and S.C. Wang, "Test Results on Adipic Acid-Enhanced
    Lime/Limestone Scrubbing at the EPA Shawnee Test Facility - Second
    Report," in Proceedings: the Fifth Industry Briefing on IERL-RTP
    Lime/Limestone Wet Scrubbing Test Programs (December 1979),
    EPA-600/9-80-032 (NTIS PB 80-199813), July 1980 (pp 27-113).

 4.  Rochelle, G.T., "The Effect of Additives on Mass Transfer in CaC03 or
    CaO Slurry Scrubbing of S02 from Waste Gases," Ind. Eng. Chem. Fundam.,
    Vol. 16, No. 1, pp. 67-75, 1977.

 5.  Rochelle, G.T., "Process Alternatives for Stack Gas Desulfurization by
    Throwaway Scrubbing," in Proceedings of Second Pacific Chemical Engineering
    Congress, Vol.1, p. 264, August 1977.

 6.  Radian Corporation, Further Study of Adipic Acid Degradation in FGD
    Scrubbers, draft final report for EPA Contract 68-02-2608, Task 72,
    April 18, 1980.

 7.  Cavanaugh, C.M., Buffer Additives for Flue Gas Desulfurization Processes,
    M.S. Thesis, The University of Texas at Austin, December 1978.

 8.  Stephenson, C.D., and R.L. Torstrick, "The Shawnee Lime-Limestone Computer
    Program," in Proceedings: the Fifth Industry Briefing on IERL-RTP Lime/
    Limestone Wet Scrubbing Test Programs (December 1979), EPA-600/9-80-032
    (NTIS PB 80-199813), July 1980 (pp 167-222).

 9.  Rochelle, G., Buffer Additives for Stack Gas Desulfurization by CaO/CaCOo
    Slurry, September 1980 Monthly Progress Report, EPA Grant R806743, EPA/IERL,
    Research Triangle Park, N.C. (R.H. Borgwardt, Project Officer).

10.  Borgwardt, R.H., et al., Limestone Scrubbing of SO? at EPA/RTP Pilot Plant,
    Progress Report 46, August 1980.
                                       285

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                                 Appendix

                       CONVERTING UNITS OF MEASURE
Environmental  Protection Agency policy is to express all measurements
in Agency documents in metric  units.   In this report, however, to avoid
undue cost or lack of clarity,  English units are used throughout.
Conversion factors from English to metric units are given below:
To Convert From

scfm (60°F)
cfm
Op
ft
ft/hr
ft/sec
ft?
frvtons per day
gal/mcf
9Pm
gpm/ftz
gr/scf
in.
in. HoO
Ib
Ib-moles
Ib-moles/hr
Ib-moles/hr ft2
Ib-moles/min
psi
                              To

                         nm3/hr (0°C)
                         nrVhr
                         °C
                         m
                         m/hr
                         m/sec
                         m;
                         FIT/roe trie  tons  per day
                         1/m3
                         1/min
                         1/min/itr
                         g/m3
                         cm
                         mm  Hg
                         9
                         g-moles
                         g-moles/min
                         g-moles/min/m2
                         g-moles/sec
                         kPa
Multiply By

    1.61
    1.70
    (°F-32)/1.8
    0.305
    0.305
    0.305
    0.0929
    0.102
    0.134
    3.79
    40.8
    2.29
    2.54
    1.87
    454
    454
    7.56
    81.4
    7.56
    6.895
                                    286

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                       COCURRENT SCRUBBER TESTS

                         SHAWNEE TEST FACILITY



                                  By

                             S.  B. Jackson
            Division of Energy Demonstrations and Technology
                            Office of Power
                      Tennessee Valley Authority
                         Muscle Shoals, Alabama
                               ABSTRACT
     Prototype cocurrent limestone scrubber tests were performed at the
Shawnee Test Facility.   The initial cocurrent prototype tests consistently
achieved greater than 90% S02 removal while operating with inlet flue gas
S0£ concentrations ranging from 1500 ppm to 3000 ppm.  Although the
prototype scrubber tower was reliable, total system reliability was not
achieved during the initial tests at 27 ft/sec superficial scrubber gas
velocity, primarily because of solids deposits in the mist eliminator and
the inline,  indirect steam reheater.   At  a 20 ft/sec superficial gas  velocity
and with low fly ash loading in the inlet flue gas there were no signifi-
cant solids  deposits in the mist eliminator or reheater.  Mist eliminator
operation was reliable during operation with high fly ash loadings and a
20 ft/sec superficial gas velocity, but the inline reheater continued to
plug with slurry solids.  During forced-oxidation tests with a single
scrubber hold tank and multiple hold tanks, operating conditions were
identified which consistently removed greater than 90% of the S0£ and
oxidized greater than 95% of the calcium sulfite in the scrubber slurry
to gypsum.
                                    287

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                       COCURRENT SCRUBBER TESTS

                         SHAWNEE TEST FACILITY
INTRODUCTION

     In 1978 the Hydro-Filter scrubber train at the Shawnee Test Facility
was modified to demonstrate the cocurrent scrubber concept.  The design
of the modification and original test program plan were based upon results
from pilot cocurrent scrubber tests conducted at the Tennessee Valley
Authority (TVA) Colbert Pilot Plant.  The initial equipment modification
and the 12-month test program (August 1978-July 1979) were funded by the
Electric Power Research Institute (EPRI) and implemented by TVA.  A second
period of cocurrent tests (August 1979-July 1980) was funded by TVA,
the Environmental Protection Agency (EPA), and the Department of Energy (DOE),
These tests were conducted to demonstrate reliable operating conditions and
limestone cocurrent scrubber operation with forced oxidation.

     This paper summarizes the results of the TVA cocurrent scrubber tests.
The highlights of the Colbert pilot plant tests and the EPRI prototype
cocurrent scrubber tests are presented as background for this discussion.
COCURRENT SCRUBBER

Background

     The cocurrent scrubber design as illustrated in Figure 1 has several
potential advantages over other commercial FGD scrubber arrangements.

  •  The equipment configuration is more compatible with most power
     plant duct and fan arrangements.  The gas enters the scrubber
     at a high elevation and leaves near ground level.  The entrainment
     separator and reheat systems (likely to require the most maintenance)
     can be near ground level.  Likewise, the induced draft (ID) fans
     can be on the ground and the connecting ductwork to the stack can
     be shorter and probably less complex.

  •  The physical arrangement of the cocurrent scrubber causes the gas
     to change direction in the base of the unit before it enters the
     mist eliminator.  Both the change in direction of the gas and the
     vertical position of the entrainment separator promote good liquid
     separation and drainage.  Also, a separate mist eliminator wash
     loop may be used, if needed.
                                    288

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                              . ELEVATION
Figure 1.  Cocurrent limestone slurry process  plan and elevation.




                                   289

-------
  •  Scrubbing liquid should coalesce into larger droplets before
     disengaging from the gas stream near the base of the scrubber
     and further facilitate efficient operation of the mist eliminator.

  •  Flooding of the unit with the associated high pressure drop and
     excessive entrainment of scrubbing slurry (even if grids are added
     to improve gas-liquid contact)  is less likely.   Also, during
     normal cocurrent operation the gas-side pressure loss is lower
     because some liquid-side energy is recovered.

  •  Higher gas velocities (small scrubbers)  are achieved because of
     the reduced tendency to flood and because more efficient mist
     elimination is likely.   Therefore, smaller or fewer scrubber
     modules would be required in a full-scale system.

     These potential advantages provided incentive for TVA and EPRI to
conduct pilot scrubber studies of the cocurrent scrubber concept with
flue gas from a coal-fired boiler at the TVA Colbert pilot plant.
Representative results from the Colbert limestone cocurrent scrubber
tests are given in Table 1.   These results and preliminary economic
studies justified prototype testing of the cocurrent scrubber at Shawnee.
          TABLE 1.   LIMESTONE COCURRENT SCRUBBER TEST RESULTS

                          COLBERT PILOT PLANT
      Inlet S02 concentration,  ppm                        2,461
      Outlet S02 concentration, ppm                         242
      Percent S02 removal                                    90
      Scrubber superficial gas  velocity, ft/sec              28
      L/G, gal/k£t3                                          69
      Limestone stoichiometry,  mol Ca/mol inlet S02        1.26
      Height of scrubber, ft                                 30
      Number of grids                                         5
      Depth of each grid, in.                                 9
      Scrubber pressure drop, in.  ^0                      15.4
     A flow diagram of the Shawnee cocurrent scrubber train as installed
for the EPRI cocurrent test program is shown in Figure 2.  The scrubber
system was designed for operation over a wide range of conditions, which
are summarized in Table 2.  Figure 3 is a schematic of the Shawnee
cocurrent scrubber arrangement.
                                    290

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                                             FLUE CAS INLET
                                   MIST
                                 ELIMINATOR
                   I
    TO INDUCED
     DRAFT FAN
ro
                   V
                          INLINE
                        REHEATER
                                            COCURRENT
                                            SCRUBBER
                                                                PRE3ATURATOR PUMP
          RIVER WATER
                                                DISPOSAL  FILTER CAKE
                                                  PUMP     RESLURRY
                                                            TANK
1

LIMESTONE
SLURRY
PREPARATION
TANK
                                     RIVER WATER
                                                                                                   LIMESTONE SLURRY
                                                                                                      FEED PUMP
A TOR
PUMP
C5-K3 C»*«3 6—
MIST ELIMINATOR SCRUBBER
-CIRCULATION CIRCULATION
TANK TANK
bCiHUHBLK LJ L_ '
CIRCULATION PUMPS 1 THICKENER
<
11
„,„, „-->. i A ,

CAKE THICKENER
f /- ,. T UNDERFLOW PUMP
BELT OR DRUM!
FILTER 1 J-~Q 	 k
1 ) — t"J! 'I
FILTRATE PUMP
          Figure ?..   Cocurrenf scrubber   Shawnnc  Steam  Plant  Test Facility -  flow diagram.
                                                                                                       RECYCLE LIQUOR  RECYCLE LIQUOR
                                                                                                        SURGE TANK     RETURN PUMP

-------
                      FLUE GAS INLET,

t
10
1
38

\
1
ft.
1
ft.
SLU
INL
2.5
RRY
ET
ft.—
i
4.2 ft.
1
— • -^z.


/\
"A




I! M 1 1

1
J
X
i
*^
J— 40" DIAMETER
- PRESAT

t
4 ft.
6 ft.
4 ft.
« >
4 .
6 ft.
-4-
4 ft.
4 > 4 .s n

/ t
/(p 4.5ft. _^
t-r-t-n «•
^"3ft- ^
                                                       BAFFLE PLATE

                                                     TO REHEATER
                                                  MIST ELIMINATOR
                                                      HOUSING
                              -.0
Figure 3.
            SCRUBBER EFFLUENT
Cocurrent scrubber,  schematic.
                    292

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           TABLE  2.   SHAWNEE  PROTOTYPE  COCURRENT SCRUBBER

                       MAJOR  DESIGN PARAMETERS


         	Design parameter	   Range

          Scrubber superficial gas velocity,  ft/sec    18-31
          L/G (at  32 ft/sec gas velocity),  gal/kft3   12-100
          Scrubber height,  ft                           25-45
          Number of spray headers                        1-4
          Number of spray nozzles/header                 4-8
          Scrubber circulation tank retention time
           at maximum recirculation rate                6-17
     Extensive testing with sodium carbonate, lime,  and limestone absorbents
was performed during the EPRI-funded program.  Detailed results of this
program were presented at the EPA Fifth Industry Briefing Conference on
Lime/Limestone Wet Scrubbing.  Representative results with each of these
absorbents are shown in Table 3.

     Highlights of the lime/limestone tests included in the EPRI test
program follow:

  •  The gas/liquor contact efficiency of the cocurrent open spray tower
     (no grids) was inadequate for S02 removal greater than 85%.

  •  Installation of grids in the tower provided effective gas and liquor
     contact, which increased the S02 removal efficiency to greater than
     90%.

  •  Slurry distribution through a single spray header at the top of the
     scrubber provided higher S02 removal than slurry distribution throughout
     the tower with multiple spray headers.

  •  Scrubber operating conditions that strongly affected S02 removal were
     gas residence time, recirculated slurry rate, and absorbent stoichiometry,
     Gas residence time had the strongest effect.  For example, at 27 ft/sec
     gas velocity and 1.0 mol Ca/mol inlet S02, the recirculated slurry
     rates required to maintain 85% S02 removal with a 25, 35, and 45. foot
     scrubber were 2370, 1780, and 1175 gpm  respectively.

  •  S02 removal by lime absorbent was slightly lower than that achieved
     in the Colbert pilot lime tests.  At similar operating conditions, the
     Shawnee scrubber achieved 93% S02 removal while the Colbert scrubber
     achieved 96% SO^ removal.
                                     293

-------
       TABLE 3.  SHAWNEE PROTOTYPE COCURRENT SCRUBBER TEST RESULTS

                            EPRI TEST PROGRAM.


                                                Absorbents
	Major test conditions	  Sodium, carbonate    Lime   Limestone

Scrubber physical configuration
  Height, ft                                 25            45         35
  Spray header location(s)
   (ft from scrubber sump)               25, 15            45         35
Flue gas
  Flow rate, aft3/min at 300°F           25,000        25,000     25,000
  Scrubber superficial gas
   velocity, ft/sec                        26.7          26.7       26.7
Slurry recirculation rate, gpm            1,440         1,200      2,400
L/G, gal/kft3                                72            60        120
Open tower or grid tower             Open tower          Grid       Grid
Scrubber pressure drop, inches ti^O          2-3             3         3
Absorbent stoichiometry
  Mols Na/mol S02 absorbed                 2.24
  Mols Ca/mol inlet S02                       -           1.1        1.3
Inlet S02 concentration, ppm              2)400         2,800      2,400
S02 removal efficiency, %                  '92            93         90
                                      294

-------
  •  During  a  350-hour  limestone  scrubbing test,  the prototype  cocurrent
    scrubber  consistently  averaged 90%  S02 removal efficiency  for  each
    successive 24-hour period.   Major scrubber operating conditions  for
    this  test were 2500 ppm inlet S02 concentration, 27  ft/sec superficial
    gas velocity,  L/G  equal to 90 gal/kft3, 8.3  inches H20 scrubber  pressure
    drop  and  limestone stoichiometry equal to 1.3 mol Ca/mol inlet S02.

  •  The scrubber tower with grids operated without scaling and plugging
    of the  tower internals; however, a  soot blower was required at the
    tower inlet to remove  solids deposits at the wet/dry interface.

  •  The total scrubber train did not operate reliably at 27 ft/sec
    scrubber  superficial gas velocity because slurry solids deposits
    plugged the mist eliminator  and reheater.


TVA  Cocurrent  Scrubber  Test Program

    After completion of the EPRI program, TVA continued  limestone  cocurrent
scrubber tests with emphasis upon improvement of  the mist eliminator  and
reheater reliability and tests with forced oxidation. The TVA  tests  were
conducted  from August 1979  to July 1980.  EPA and DOE provided  funds  for
the  test program after  June 1. The test program was separated  into two
primary test blocks:

  •  Mist  eliminator reliability  tests

  •  Forced-oxidation tests
     Mist Eliminator Reliability Tests.   These tests were performed to
determine operating conditions that would provide reliable mist  eliminator
and reheater operation.   Velocity profile determinations upstream and
downstream of the mist eliminators indicated that the gas distribution
at the mist eliminator entrance was very poor (see Figure 4).  The plans
for the reliability tests were based primarily upon the hypothesis that
improvement of the gas distribution at the outlet of the scrubber and the
entrance to the mist eliminators would improve the mist eliminator relia-
bility and efficiency.  Improved mist eliminator efficiency would in turn
improve the reheater reliability.

     Scrubber operating conditions and scrubber equipment were revised
during this test block as follows:

  •  The scrubber superficial gas velocity was lowered from 27 to 20
     ft/sec.

  •  The flue gas source was changed from upstream of the boiler ESP to
     downstream of the ESP.

  •  The solids concentration in the recirculated scrubber slurry was
     reduced from 15% to 10%.
                                   295

-------
rss
                 Average = 23
                         Second-Stage
                         Mist Eliminator
                         Four-Pass
First-Stage
Mist Eliminator
Three-Pass
                 NOTE:  The calculated velocity is 18.5 ft/sec In the mist eliminator duct
                      and 22 ft/sec in the vertical duct.
                                                                    Average = 28
7VX
  I  '/ y 3x
\HX68yf29;^22
18
                                        A
                                                                                        s
                                                                                                  iO
                Figure A.   Cocurrent scrubber mist  eliminator  velocity  profile  (ft/sec).   Air  only at  a
                             scrubber superficial gas  velocity of 27 ft/sec.

-------
  •  Presaturator spray nozzles and a soot blower for solids cleaning
     were installed at the inlet of the scrubber.

  •  A 3-pass,  open-vane mist eliminator was installed in the outlet
     duct of the scrubber sump and turning vanes, were installed in
     the 90-degree turn immediately upstream of the mist eliminator.

All of these revisions, except the presaturator installation, were made
to decrease the amount of solid and liquid entrainment leaving the scrubber
(entering the mist eliminator) and to improve the entrainment removal
efficiency of the mist eliminator.  Operating conditions and results of
this test series are summarized in Table 4.  All tests, except test LS-4100C,
were performed with low fly ash loading in the flue gas.  Tests LS-5000C,
5001C, and 5002C were performed with a 20 ft/sec scrubber gas velocity and
tests LS-5010C and 4100C were performed with a 27 ft/sec gas velocity.  The
presaturator sprays were installed before test LS-5001C.  The open-vane
mist eliminator and turning vanes were installed before test LS-4100C.

     Highlights of these tests are summarized as follows:

  •  Reduction of the scrubber superficial gas velocity to 20 ft/sec
     and the fly ash loading to 'U).! gr/sft^ essentially eliminated
     solids deposits in the mist eliminator and reheater.

  •  Maximum localized gas velocities in the mist eliminator were
     reduced from 50-60 ft/sec to 35-40 ft/sec when the scrubber gas
     velocity was reduced from 27 to 20 ft/sec.  (The mist eliminator
     vendor claims high entrainment removal efficiency at 35 to 40 ft/sec.)

 . •  Solids deposited in the mist eliminator and reheater while operating
     at 27 ft/sec scrubber gas velocity and low fly ash loadings.

  •  Solids deposits at the wet/dry interface were controlled by periodically
     cleaning the area around the presaturator spray nozzles with a soot
     blower.

  •  The open-vane mist eliminator and the turning vanes that were installed
     at the outlet of the scrubber did not impr.ove the mist eliminator
     and reheater reliability while operating the scrubber at a 27 ft/sec
     gas velocity.

     Further testing at 27 ft/sec scrubber gas velocity was postponed to
permit forced-oxidation tests at 20 ft/sec*  Future tests at a higher gas
velocity (V30 ft/sec) will be conducted after the scrubber outlet duct is
modified to provide better gas distribution in the mist eliminator.


     Limestone Cocurrent Scrubber Tests with Forced Oxidation (Single Tank
Mode).  Limestone scrubbing tests with forced oxidation began in October
1979.  The first series of tests was performed with air sparging and limestone
                                    297

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ID
00
                                             TABLE 4.  HIGHLIGHTS OF TVA LIMESTONE MIST ELIMINATOR RELIABILITY TESTS

                                                                       COCURRENT SCRUBBER
Test Nuinber
On-stream time, hr
Scrubber operating conditions
Physical configuration
Height, ft
Number of grids3 >D
Header location0
Pressure drop, in. ^0
Flue gas
Flow rate (inlet), aft3/min (300°F)
Superficial velocity at 125°F, ft/sec
Inlet S02 concentration, ppm
Slurrye»f
Recirculation rate, gpm
L/G, gal/kft3
Laboratory results
Recirculated slurry
Solids concentration, wt %
pH
Total dissolved solids, ppm
Solids
Stolchlometry, mols Ca/mol inlet 803
Thickener underflow
Solids concentration, wt %
Filter cake
Solids concentration, wt %
S02 removal efficiency, %
LS-5000C
319


38
6
B
3.5-A.O

18, 750
20.0
1,340-2,120

1,400
93


8.3-11.5
6.0-6.4
4,100-9,900

. 1- 12- 1.46:

18.8-27.4

54.9-77.2
88-94
LS-5001C
470


38
6
B
3.3-4.3

18,750
20.0
1,320-2,320

1,495
100


8.2-11.5
5.93-6.43
2,440-11,295

1,16-1.52

16.1-23.0

54.7-78.7
92-94
LS-5002C
348


38
6
B
3.3-4.3

18,750
20.0
1,840-2,440

1,495
100


8.7-11.4
5.83-6.40
7,618-17,708

1.18-1.52

18.1-27.4

56.5-67.3
92-94
LS-5010C
238


38
6
B
6.6-7.9

25,000
27.0
1,360-2,680

1,895
95


8.7-11.4
5.85-6.29
9,423-15,144

1.16-1.47

13.6-21.9

54.7-62.5
93-97
LS-4100C
170


38
6
B
7.0-8.5

25,000d
27.0
2,000-2,680

1,895
95


14.8-16.2
5.84-6.17
5,500-9,545

1.23-1.44

24.9-30.0

54.3-59.6
92-95

                       a.   Grid elevations:   402,  398,  392,  388, 382,  and 378 ft.
                       b.   Depth of grids was 3-3/4 inches/elevation.
                       c.   Header elevation:   B, 407 ft.
                       d.   Flue gas with full loading of  fly ash.   All other tests used flue gas with low loading of fly ash.
                       e.   Includes presaturator slurry.
                       f.   Scrubber recirculation tank slurry depth was 6 ft for all tests except test LS-4100C which was 16.
5 ft.

-------
addition in a single scrubber circulation tank as shown in the flow diagram
in Figure 5.  The scrubber internal arrangement and the range of major
operating conditions for this first series are summarized in Table 5.
        TABLE 5.  MAJOR COCURRENT SCRUBBER OPERATING CONDITIONS

            LIMESTONE SCRUBBING TESTS WITH FORCED OXIDATION

                           SINGLE TANK MODE
         Flue gas flow rate  (inlet)   18,750 a.ft3/min at 300°F
         Scrubber gas velocity              20 ft/sec at 125°F
         Recirculated slurry rate, gpm                    1500
         L/G, gal/kft3                                     100
         Recirculated slurry solids
          concentration, %                               10-15
         Scrubber height, ft                               38
         Limestone stoichiometry,
           mols Ca/mol inlet S02                           1.3
         Grids                                               6
         Depth of each grid, inches                      3-3/4
         Air stoichiometry,
          Ib-atoms 0/lb-mol  S02 absorbed                2.0-4.0
     The objective of  this  test block was  to  define  operating  conditions
 that would simultaneously achieve  90% SOo  removal  and  oxidize  greater than
 90% of  the calcium sulfite  in  the  recirculated  slurry  to  calcium  sulfate
 dihydrate.  Initially  screening tests were made to study  the effect  of
 oxidation air rate on  the scrubber S02  removal  efficiency and  the degree
 of oxidation.  The operating conditions and results  of these tests are
 presented in Table 6.   The  S02 removal  efficiency  and  percent  oxidation
 during  several of these tests  are  briefly  summarized below:
Test number LS-                    5120C    5121C   5122C   5140C    5130C

Limestone stoichiometry,
 mols Ca/mol inlet S0£                1.3      1.3    1.3      1.1      1.1
Oxidation air stoichiometry,
 Ib-atoms 0/lb-mol S02 absorbed   1.6-2.4  2.6-3.2    2.5  2.3-3.1  2.8-3.7
S02 removal efficiency, %           93-97    87-96  88-96    72-85    88-94
Slurry solids oxidation, %          60-81    95-99  66-87   99-100   99-100
                                    299

-------
                                                   FLUE  GAS INLET
    TO INDUCED A-.
     DRAFT FAN\J,
co
o
o
                                                                        PRESATURATOR PUMP
'

LIMESTONE
SLURRY
PREPARATION
TANK
                                                                                                       RIVER WATER
             WIST. ELIMINATOR
            CIRCULATION PUMP
           RIVER WATER
+ '
o-
*
0
f


ST .ELIMINATOR
CIRCULATION
^ t
J *
sc
CIR
1
*
'o

-------
                       TABLE 6.  HIGHLIGHTS OF TVA LIMESTONE COCURRENT SCRUBBER TESTS WITH FORCED OXIDATION - SINGLE TANK MODE
Operating Period
Test Number
Ons Cream time, hr
Scrubber operating conditions
Physical configuration
Height, ft
Number of stages'*
Number of grids per stagec
Header location''
Pressure drop, in. H-0
Flue gas ,
Flow rate (inlet), af t /mln at 300°F
Superficial velocity ^ ft/sec at 125°F
Inlet S0_ concentration, ppm
S lurry f
Reclrculation rate, gpm
L/G, gal/kaft3
Scrubber circulation tank conditions
Physical configuration
Slurry depth, ft
Agitator speed, rpm
Oxidation air
Rate, sft3/min
Stoichiometry, Ib-atoms 0/lb-mo] SO^ absorbed
Laboratory results
Recirculated slurry
Solids concentration, vt %
PH
Liquor
Total dissolved solids, ppm
Sulfite concentration, ppm
Oxidation, %S
Solids
Stoichiometry, mols Ca/mol inlet SQ2
Oxidation, %8
Thickener underflow
Solids concentration, wt %
Filter cake
Solids concentration, wt %
S0_ removal efficiency, %
Oct. 24-26
LS-5100C*
47


38
6
3
B
3.2-3.6

18,750e
20.0
1,360-1,680

1,495
100


10
45

100
2.1-3.0


4.8-8.0
5.9-6.1

5,072-10,107
63-145
92-96

1.20-1.38
41-48

12.0-13.7

-
92-94
Dec. 13-23
LS-5110C"
250


38
6
3
B
3.4-4.3

18,750
20.0
2,140-3,300

1,495
100


16.5
68

250
2.8-4.0


13.6-17.0
5.6-6.1

5,724-15,618
16-152
92-99

1.18-1.50
98-100

18.4-27.3

54.9-89.0
90-94
Dec. 27-Jan. 2
LS-5120(y
136


38
6
3
B
3.5-4.0

18.750
20.0
2,120-3,200

1,495
100


16.5
68

150
1.6-2.4


13. 1-1*. 7
5.9-6.4

5,368-7,253
9-163
90-99

1.31-1.47
60-81

17.4-30.0

65.4-80.3
93-97
Jan. 2-10
LS-5121C"
192


38
6
3
B
3.7-4.3

18, 750
20.0
2.260-3,320

1.495
100


16.5
68

200
2.6-3.2


13.4-17.0
5.5-6.2

5,428-8,652
45-253
85-98

1.18-1.35
95-99

22.6-39.0

63.9-85.3
87-96
Jan. 10-15
LS-5130C8
118


38
6
3
B
3.8-4.5

18,750
20.0
1,960-2,800

1,695
113


16.5
68

200
2.8-3.7


13.0-17.1
5.6-5.9

7,242-9,642
7-76
95-100

0.98-1.12
99-100

16.3-33.5

78.8-89.7
88-94
Jan. 15-21
LS-5140C3
140


38
6
3
B
3.6-4.3

18,750
20.0
1.900-2,600

1,695
113


16.5
68

1-50
2.3-3.1


13.5-16.6
5.0-5.5

7,488-11,278
416-1,402
49-94

1.08-1.34
99-100

19.5-27.3

76.0-92.4
72-85
Jan. 23-31
LS-5122C
178


38
6
3
B
3.3-4.0

18,750
20.0
1,820-2,720

1,495
100


16.5
68

_
2.4-2.7


14.0-16.1
5.7-6.3

5,500-8,398
34-136
91-98

1.11-1.43
66-87

18.2-31.7

67.8-79.2
88-96
    Turning vanes and open-vane mist eliminator were installed in the 90-degree elbow upstream of  the  mist  eliminator housing.
b.  Grid elevations:  402, 398, 392, 388, 382, and 378 ft.
c.  Depth of each grid was 1-1/4 inches.
d.  Header elevation:  B, 407 ft.
e.  Flue gas with low-loading of fly ash.  All other tests were with flue gas with full-loading of fly ash.
f.  Includes 85-95 gpm for presaturator; remaining slurry distributed through six 3-inch,  60-degree spray angle Bete nozzles  (ST128TTCN) located at
    B-header.
g.  Percent of total sulfur present aa sulfate.
                                                                      (continued)

-------
                                                             TABLE 6  (continued)
Operating Period
Test Number
Onstream time, hr
Scrubber operating conditions
Physical configuration
Height, ft
Number of stages3
Number of grids per stage1"
Header- location0
Pressure drop, in- H^O
Flue gasd ,
Flow rate (inlet), aft /min at 300°F
Superficial velocity, ft/sec at 125°F
Inlet S0~ concentration, ppm
Slurry6
Recirculation rate, gpm
L/G, gal/kaft3
Scrubber circulation tank conditions
Physical configuration
Slurry depth, ft
Agitator speed, rpm
Oxidation air
Rate, sft3/min
Stoichiometry , Ib-atoms 0/lb-mol 862 absorbed
Laboratory results
Recirculated slurry
Solids concentration, wt %
pH
Liquor
Total dissolved solids, ppm
Sulfite concentration, ppm
Oxidation, %f
Solids
Stoichiometry, tnols Ca/mol inlet S02
Oxidation, Xf
Thickener underflow
Solids concentration, wt %
Filter cake
Solids concentration, wt %
SO removal efficiency, %
Jan. 31-Feb. 5
LS-5123C
119


38
6
3
B
3.4-3.9

18,750
20.0
2,200-2,560

1,495
100


16.5
68

_
2.8-3.1


14.3-16.7
6.0-6.2
5,714-10,531
•36-100
93-97

1.30-1.38
82-92
20.8-39.4

53.7-78.6
91-95
Feb. 7-28
LS-5124C
449


38
6
3
B
3.5-4.6

18,750
20.0
2,100-3,000

1,495
100


16.5
68

_
3.2-3.6


12.3-17.1
5.5-6.1
4,235-9,935
18-470
80-99

1.18-1.51
92-99
19.2-31.1

73.7-87.7
87-93
Feb. 29-Mar. 11
LS-5150C
228


38
6
6
B
6.9-8.2

18,750
20.0
2,140-3,120

1,495
100


16.5
68

-
2.3-2.7


13.1-16.7
5.0-6,1
4,523-10,401
145-1,031
69-92

0.98-1.32
85-96
15.6-39.4

70.1-87.5
73-90
Mar. 11-13
LS-5151C
64


38
6
6
B
8.8-9.4

18,750
20.0
1,900-2,480

1,885
126


16.5
68

_
2.4-2.7


13.9-16.4
5.0-5.3
9,524-11,144
14-510
75-99

0.98-1.18
99
23.2-33.7

78.4-80.7
89-93
Mar. 14-21
LS-5160C
118


38
6
6
B
8.3-9.1

18,750
20.0
1,880-2,540

1,885
126


16.5
68

-
3.3-3.9


13.9-17.4
5.1-5.7
8,800-12,890
7-118
90-99

0.99-1.21
98-100
16.4-31.0

85.8-89.0
90-95
Mar. 21-26
LS-5161C
115


38
6
6
B
8.4-9.1

18,750
20.0
2,160-2,600

1,885
126


16.5
68

_
2.9-3.2


13.9-16.3
5.4-5,8
8,725-12,852
18-45
96-99

1.03-1.26
99-100
22.3-34.2

78.1-90.6
94-96
a.  Grid elevations:  402, 398, 392, 388, 382, and 378 ft.
b.  Depth of each grid was 1-1/4 inches,
c.  Header elevation:  B, 407 ft.
d.  Flue gas with full-loading of fly ash.
e.  Includes 85-95 gpm for presaturator; remaining slurry distributed through six 3-inch, 60-degree spray angle Bete nozzles (ST128FFCN) located at
    B-header.
f.  Percent of  total  sulfur present as  sulfate.

-------
These  tests demonstrated the degree of difficulty associated with simul-
taneously achieving greater than 90% S02 removal and greater than 90%
oxidation.  In several of the tests, particularly LS-5140C, limestone
blinding apparently occurred and the S02 removal efficiency of the scrubber
decreased.  This phenomenon has been explained by the hypothesis that
high liquor sulfite concentration (1400 ppm 803 in test LS-5140C) and low
solid-phase sulfite concentration combine to promote precipitation of
calcium sulfite on the surface of the limestone.  If this occurs, the
limestone dissolution rate, the overall rate-controlling mechanism of
this process, decreases and, consequently, the S02 removal efficiency
drops.

     Laboratory analyses  (scanning electron microscope examination) clearly
indicate that the limestone in the slurry from these tests is not physically
blinded.  Limestone addition to the scrubber circulation tank during these
tests did not, however, provide the expected increase in slurry pH and
S02 removal efficiency.   Further laboratory investigation is needed in an
attempt to fully explain  this process problem.

     The next series of tests (LS-5155, -5200, -5210, and -5201) were
performed with the air stoichiometry controlled at 3.0 Ib-atoms 0/lb-mol S0£
absorbed.  The limestone  stoichiometry was varied from 1.1 to 1.3 mol
Ca/mol inlet S02-  Also,  after test LS-5155, the depth of the.grids in the
•scrubber was increased from 3-3/4 to 7-1/2 inches.  Operation with thicker
grids permitted a decrease in L/G to 85 gal/kft3 without reducing the S02
removal below 90%.  The major operating conditions and results of this test
series are summarized in  Table 7.  The performance of the scrubber is briefly
summarized below:


Test number LS-               5155         5200         5210         5201

.Mode                       Single-tank  Single-tank  Single-tank  Single-tank
Inlet S02 concen-
  tration, ppm              2,060-2,600  1,960-2,600  1,800-2,640  1,560-2,480
S0£ removal
  efficiency, %                      97        90-93        91-94        90-94.
Limestone stoichiometry-
  mols Ca/mol inlet S02       1.11-1.16    1.08-1.18    1.20-1.49    1.06-l.lj
Air stoichiometry, Ib-atoms
  0/,lb-mol S02 absorbed         2.9-3.2      2.9-3.2      2.8-3.2      2.7-3.2
Liquor to gas ratio,
  gal/kft3                          126           87           85            85
Scrubber pressure drop,
  inches H20                   8.4-10.7      6;3-7.0      6.4-7.3      6.2-7.0
Oxidation, %
  1 Liquor phase                   87-98        88-98       90-100       86-100
  Solid phase                   99-100       98-100       99-100       99-100


     All of these tests consistently achieved greater than 90% S02 removal  and
greater than 97% oxidation of the slurry solids.  Apparently the higher air
stoichiometry prevented limestone blinding during these tests.
                                    303

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TABLE 7.   HIGHLIGHTS OF TVA LIMESTONE  TESTS WITH FORCED OXIDATION IN A  SINGLE TANK MODE
Operating Period




Test Number
                                           Apr11 3°-May 5   *** 5~May 9   May ')-™sy 16   May "'^ 20




                                              LS-5155         LS-52°°       LS-521°         LS-5201
Onstream time, hr
Scrubber operating conditions
Physical configuration
Height, ft
Number of stages8
Number of grids per stage"
Header location0
Pressure drop, in. ^0
Flue gas**
Flow rate (inlet) . af t3/min at 300°F
Superficial velocity, ft/sec at 125°F
Inlet SC>2 concentration, pptn
Slurry6
Recirculation rate, gpm
L/G, gal/kaft3
Make-per-pass, milli-g-mol S02 absorbed /liter slurry
Scrubber circulation tank conditions
Physical configuration
Slurry depth, ft
Agitator speed, rptn
Oxidation air
Rate, sft3/min
Stoichiometry, Ib-atoms 0/lb-mol S02 absorbed
Laboratory results
Recirculated slurry
Solids concentration, wt %
pH
Liquor
Total dissolved solids, ppm
Sulfite concentration, ppm
'Oxidation, %f
Solids
Stoichiometry, mols Ca/mol inlet S02
Limestone utilization, %
Oxidation, %f
Thickener underflow
Solids concentration, wt %
Sludge cake
Solids concentration, wt %
S02 removal efficiency, %
a. Grid elevations: 402, 398, 392, 388, 382, and 378 ft.
b. Depth of each grid was 1-1/4 inches.
c. Header elevation: B, 407 ft.
d. Flue gas with full loading of fly ash.
e. Includes 65-100 gpm for presaturator; remaining slurry
nozzles (ST128FFCN) located at B-header.
f. Percent of total sulfur present as sulfate.
7 1
3$
6

8.4-10.7
18,750
20.0
2,060-2,600

1,885
126
4.3-5.1


16.5
68

190-210
2.9-3.2


13.8-16.8
5.2-5.8

8,040-9,953
45-167
87-98

1.11-1.16

99-100

25.5-33.7

81.5-89.3
97




distributed


38
&
g
g
6.3-7.0
18,750
20.0
1,960-2,600 1

1,300
87
5.5-7.1


16.5
68

160-200
2.9-3.2

1
12.1-17.3
5.2-5.6

5,013-13,917 8,
23-158
88-98

1.08-1.18
76.9-83.3-
98-100

15.Z-37.9

77.5-89.7
90-93




through six 3-inch,


38
6
5
B
6.4-7.3
18,750
20.0
,800-2,640

1,270
&5
4.9-7.3


16.5
68

150-200
2.8-3.2


11.2-16.6
5.4-5.9

530-15,366
0-136
90-100

1.20-1.49.
62.5-76.9
99-100

18.7-41.1

79.3-87.7
91-94




, 60-degree


38 .
6
6-
B
6.2-7.Q .
18,750" -
20.0'
1,560-2,480

1,265
85
4.9-7.0


14.5
68

140-190
2.7-3.2


13.3-16.8
5.4-5.8

10,479-15,922
0-158
86-100

1.06-1. i:i
71.4-85.1
99-100

19.6-26.3

76.4-82.0
90-94




spray angle Bete.


                                          304

-------
     The percent solids in the gypsum filter cake produced during these
tests varied from 76% to 90%.  A typical composition of the solids produced.
is summarized below:

                                     Weight % (dry)

                                          59.5
                    CaS03-l/2H20           0.1
                    CaC03                 13.4

                    Fly ash               27.0

The settling rate of the solids varied from about 0.1 cm/min at 65% oxidation
to 1.0-2.5 cm/min near complete oxidation.  Figure 6 is a plot of the solids
settling rate versus percent oxidation, which was generated from solid
settling tests performed with oxidized slurry from all of the cocurrent
scrubber forced-oxidation tests.
     Limestone Cocurrent Scrubber Tests with Forced-Oxidation (Multiple
Tank Mode).  Following the single tank mode tests, the scrubber circulation
equipment was modified to permit operation with multiple hold tanks.  A
flow diagram of the scrubber train in the multiple tank mode is shown in.
Figure 7.  Potential advantages of this mode of operation are:

  •  A lower pH for the oxidation reaction

  •  Liquor compositions less likely to promote limestone blinding

  •  Improved limestone utilization

In this operational mode air is sparged into the first tank, which receives
the scrubber effluent.  The lower pH of the effluent should provide improved
oxidation air utilization because calcium sulfite solubility increases as
fhe pH decreases.  Addition of limestone in the second tank after the slurry
liquor is oxidized and the liquor sulfite concentration is low should prevent
limestone blinding.  The multiple tank arrangement partially simulates plug
flow and should improve the limestone utilization.

     Five forced-oxidation tests that were performed in this test series
are summarized in Table 8.  Although additional parametric tests should
have been performed, an extended period of operation was required for the
reliability demonstration test, LS-6150, before the test program was discon-
tinued in July.

     In tests LS-6100, -6110, and -6120, the oxidation air stoichiometry was
controlled at 3.0, 2.5, and 2.0 Ib-atoms 0/lb-mol S02 absorbed, respectively,
while other process control points remained constant, including the limestone
stoichiometry at 1.1 mpl Ca/mol S02 absorbed.  (Test LS-6100B was a repeat of:
                                     305

-------
•H



"a
u
g
oo



5«
3
g
PQ


§
O

oo
      0.5 —
                          70
      80



OXIDATION, %
90
100
   Figure 6.  Limestone scrubbing slurry  settling rate versus percent

              oxidation.
                                    306

-------
                                          FLUE GAS INLET
 TO INDUCED
 DRAFT FAN
t*>
O
\

LIMESTONE
SLURRY
PREPARATION
TANK
RIVER WATER
                                                                 BACK MIX PUMP  PRESATURATOR PUMP
                                                                                           THICKENER
                                                                                        UNDERFLOW PUMP
        RIVER WATER
                           TO POND DISPOSAL

                                            DISPOSAL  FILTER CAKE
                                              PUMP   RESLURRY
                                                       TANK
                                                                                                  RECYCLE LIQUOR RECYCLE LIQUOR
                                                                                                    SURGE TANK    RETURN PUMP
          Figure 7.   Cocurrent scrubber, Sha-vnce Test  Facility - flow  diagram  for forced-oxidation
                       test <= - lu^l-ciple  hold tan" -•

-------
TABLE 8.   HIGHLIGHTS  OF TVA LIMESTONE COCURRENT SCRUBBER TESTS




                     WITH FORCED  OXIDATION




                      MULTIPLE  TANK MODE
Test number LS-
On-stream time, hr
Limestone stoichiometry,
mols Ca/mol inlet S02
Air stoichiometry, Ib-atoms
0/lb-mol S02 absorbed
Scrubber L/G, gal/akft3
Limestone utilization, %
Scrubber outlet slurry,
pH
Liquor
Sulfite concentration,
ppm
Oxidation, %
Solids
Oxidation, %
Recirculated slurry,
PH
Solids oxidation, %
Liquor oxidation, %
Liquor sulfite concentration.
ppm
S02 removal efficiency, %
6100
143

1.0-1.2

2.8-3.2
85-97


5.2-5.4


160-500
74-92

99.6-100

5.8-6.3
98-100
88-100
t
0-181
89-92
6110
150

1.07-1.10

2.3-2.7
98
83-91

5.3-5.9


68-588
71-96

99.6-100

5.9-6.3
99-100
95-100

0-172
89-93
6120
24

1.04-1.2

2.0
98
77-83

5.3


814
68

99.6

5.6-6.1
99.6
83-97

45-339
89-91
6100B
40

1.07-1.1

2.9-3.1
98
83

5.3-5.4


339-452
79-84

99.5-100

6.0-6.2
99.6-100
98.5-99.4

9-68
89-91
6155
692

1.18-1.42

2,8-3.2
. 98
; 67-77

5.3-5.6


279-598;
72-87

98-100

5.7-6.4
94-100
87-10C

0-139
92-95
                             308

-------
LS-6100.)  Operating conditions for the reliability demonstration were
selected to ensure that the scrubber SC>2 removal efficiency and percent
oxidation were maintained above 90% and 95%, respectively.

     Major conclusions and observations from the multiple tank forced-
oxidation .tests and the reliability demonstration include:

  •  90% S02 removal efficiency and percent oxidation greater than
     98% can be consistently achieved.

  •  The multiple tank arrangement for these tests does not provide
     improved limestone utilization.  (There appeared to be a slight
     decrease in limestone utilization, compared with single tank
     mode with forced oxidation.  Additional tests are needed to
     determine the cause of this unexpected result.)

  •  Oxidation air utilization is improved in the multiple tank mode.
     Greater than 95% oxidation was achieved in both the liquor and
     solid phases of the slurry while operating with 1.1 mol Ca/mol
     inlet S02 and 2.5 Ib-atoms 0/lb-mol S02 absorbed.  The single tank
     mode required 3.0 Ib-atoms 0/lb-mol S02 to achieve these conditions.

  •  Conditions which promote limestone blinding (high 803 concentration
     in  the slurry liquor and high percent oxidation of the slurry solids)
     did not develop until the oxidation air stoichiometry was reduced
     to  2.0.  Limestone blinding occurred with the air stoichiometry
     controlled at 2.5 during single mode tests.

  •  The demonstration confirmed the long-term reliability and efficiency
     of  the scrubber tower.  The S02 removal efficiency was 92% to 95%
     and the percent oxidation was 98% to 100% during, this 700-hour period.

  •  Although there were no significant solids deposits in the scrubber
     tower or mist eliminator, the reheater plugged with slurry solids.
     The deposits in the reheater apparently were caused by higher fly
     ash loadings in the flue gas (and the resulting higher recirculated
     slurry density) than were present in the earlier successful relia-
     bility demonstration.  Additional tests are needed to define operating
     conditions that do not cause plugging of the inline reheater.


     Conclusions.  Table 9 is a summary of major design criteria for a
 cocurrent scrubber system.  These criteria apply primarily to the scrubber
 area and are based upon the results of tests at Shawnee.
                                    309

-------
    TABLE 9.  MAJOR DESIGN CRITERIA FOR LIMESTONE

      COCURRENT SCRUBBER WITH FORCED OXIDATION


	Parameter	

Inlet S02 concentration, ppm                    2,400
Percent S02 removal                                90
Scrubber superficial gas velocity, ft/sec          20
L/G, gal/kft3                                      98
Limestone stoichiometry, mol Ca/raol inlet S02     1.3
Number of grids                                     6
Height of each grid, inches                       7.5
Scrubber AP, inches H20                           7.0
Total system AP, inches ^0                      13.0
Scrubber height, ft                                38
Grid spacing, ft                                    5
Oxidation tank residence time, min                  5
Hold tank residence time, min                      10
Air stoichiometry, mols 02/mol S02 removed        1.5
Oxidation efficiency, %                            99
Percent solids in throwaway gypsum sludge          80
                          310

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                           DOWA PROCESS TESTS

                          SHAWNEE TEST FACILITY



                                   By

                              S. B. Jackson
            Division of Energy Demonstrations and Technology
                             Office of Power
                       Tennessee Valley Authority
                         Muscle Shoals, Alabama

                               C. E. Dene
                    Coal Combustion Systems Division
                    Electric Power Research Institute
                         Palo Alto, California

                              D. B. Smith
                         Air Correction Division
                               UOP, Inc.
                          Des Plaines, Illinois
                                ABSTRACT

     Dowa dual-alkali process tests at the Shawnee Test Facility were
the first application of the Dowa process with flue gas from a coal-fired
boiler.  The operating conditions were based on operating experience at
Dowa facilities at smelter plants, sulfuric acid plants, and oil-fired
steam generator plants in Japan.

     The initial tests utilized the existing Turbulent Contact Absorber
(TCA) in the Shawnee train 200.  The maximum S02 removal efficiency by the
TCA was 85% to 90%.  During the TCA testing, problems with gas flow distri-
bution in the absorber were observed.  Subsequently, the mobile sphere
packing in the TCA was replaced with rigid packing to improve gas flow
distribution and gas liquid contact.  A factorial absorption test series
was conducted using the rigid packing.  As a result, operating conditions
which will consistently achieve greater than 90% S02 removal efficiency
were identified.

     Performance of the neutralization and gypsum dewatering process steps
was generally satisfactory during the absorption tests.

     Extensive reliability tests were not conducted; however, no significant
reliability problems were identified during the factorial absorption tests.
                                     311

-------
                           DOWA PROCESS TESTS

                          SHAWNEE TEST FACILITY
INTRODUCTION

     The Dowa process is a dual-alkali flue gas desulfurization (FGD)
process which utilizes basic aluminum sulfate solution for SC^ absorption
and limestone for regeneration of the absorbent.  The process was developed
by the Dowa Mining Company of Tokyo, Japan, and will be marketed in the
United States by the Air Correction Division of UOP, Inc.  The process
is now in commercial operation in Japan at an oil-fired boiler, smelters,
and sulfuric acid plants.  The Shawnee prototype Dowa installation is
the first test of the Dowa process with flue gas from a coal-fired
boiler.

     Potential advantages of the Dowa process over the conventional
limestone scrubbing process which were justification for the Shawnee
tests are:

  •  Utilizes clear solution scrubbing versus slurry scrubbing to eliminate
     erosion of equipment and slurry solids buildup on mist eliminator
     and absorber internals.

  •  Requires lower limestone stoichiometry.

  •  Produces a gypsum byproduct which has better dewatering characteristics
     than unoxidized limestone scrubbing sludge.  The Dowa gypsum may be
     used for wallboard production.

     Additional requirements of a Dowa system as compared to a conventional
limestone scrubbing system are as follows:

  •  Includes more equipment and is more complex than a conventional
     single-loop scrubbing system (excluding sludge mixing and fixation
     equipment when required as a part of a limestone system).

  •  Uses an absorbing solution pH of approximately 3 compared to 5 to 6
     for a limestone scrubbing system.  At the lower pH more acid-
     resistant materials of construction are required.  In areas where
     carbon steel or a low alloy steel is  used in a limestone system,
     316L or 317L stainless steel or epoxy resin-lined carbon steel is
     required.
                                     312

-------
     The Shawnee Dowa process test program was a jointly funded project
by the Electric Power Research Institute (EPRI) , the Tennessee Valley
Authority (TVA), and UOP, Inc.  The final month of tests was funded by the
Environmental Protection Agency (EPA).  The primary purpose of the
program was to demonstrate that the process can effectively treat flue
gas from a coal-fired boiler.  Shawnee train 200, a TCA scrubber system,
was modified to the Dowa process configuration and an 8-month test
program was conducted.  The original program plan included:

 1,  A 1-month process equipment shakedown and process demonstration at
     operating conditions recommended by Dowa and UOP.

 2.  Factorial tests of the absorption process step.

 3.  Factorial tests of the neutralization and dewatering process
     steps.

Due to problems with process  control and major equipment problems which
caused lengthy delays, the neutralization and dewatering tests were
eliminated from the test program.  However, the neutralization and
dewatering sections were operated  continuously during all of the tests.

Process Chemistry

     The overall chemical reactions in each of the major process steps
are:

   •  Absorption:       A12(S04)3-A1203 + 3S02 ->• A12(S04)3-A12(S03)3     (1)

   •  Oxidation:    A12
-------
     Al+3 + x OH' J Al(OH)+(3-x)                                       (7)
+(3~X) + H+ J H0 + AKOH)"                                (8)
     Al(OH)
           x                              -

     Oxidation

           + 1/202 + H+ + S04~2                                        (9)


     Neutralization

     SO"2 + CaC00(s) + 2H00 •*• CaSO.-2H90  (s)  + + CO "2               (10)
       4         J        £        q-   /            -5

     C03~2 + H20 J HC03~ + OH~                                        (11)


     HC03~ + H20 J H2C03 + OH~                                        (12)
     H2C03 (diss.) t H20 + C02(diss.) ? C02(g)                        (13)


     The last reaction goes to completion at pH  3.

     In summary, sulfur dioxide is absorbed in a solution of  basic
aluminum sulfate at a pH of approximately 3 [reactions  (4)  through (8)].
The resultant sulfite in the liquor is oxidized  to  sulfate by oxygen in the
flue gas and in the air which is sparged into the liquor  [reaction (9)] .
The oxidized liquor is regenerated to basic aluminum sulfate  by neutrali-
zation with limestone [reactions (10) through (13)].  The gypsum byproduct
from the neutralization step is removed by gravitational  settling and
filtration.  The filtrate and clarified liquor are  returned to the process.

     High S02 removal by the process requires the equilibrium of reaction  (5)
be shifted to the right to allow more HS03~ in solution.   This is accomplished
by more efficient oxidation of the absorber liquor  [reaction  (9)].

     The concentrations of chloride and magnesium in the  process liquor
are controlled by a purge stream.  The aluminum  content of the purged liquor
is recovered by adding excess limestone to precipitate  the aluminum as
aluminum hydroxide.  The precipitated aluminum is separated from the super-
natant liquor and returned to the process.  (Equipment  for aluminum recovery
was not installed at Shawnee.)

     Control of the process chemistry requires measurement and control of
the total aluminum concentration in the process  liquor  and the percentage
of this aluminum available for the S02 absorption reactions.   The aluminum
concentration is monitored by routine laboratory analysis and controlled by
addition of aluminum sulfate solution to the absorber hold tank.  The
percentage of the aluminum available for absorption is  controlled by
measurement and control of "% basicity."  The concept of  % basicity is
defined in the following discussion.
                                     314

-------
     Basic aluminum sulfate solution, the absorbent for the Dowa process,
is prepared by reacting solutions of aluminum sulfate with limestone to
remove sulfate as precipitated gypsum.  The. limestone is added in less
than stoichiometric amounts to prevent converting the aluminum to aluminum
hydroxide, which would precipitate.  Curve A of Figure 1 shows the pH
behavior of an aluminum sulfate solution titrated with either standard
acid or standard base.  Curve B of Figure 1 shows the behavior of an
aluminum sulfate solution that is titrated by incremental additions of
powdered calcium carbonate.  These results are plotted using the same
abscissas as Curve A.  The differences between Curve A and Curve B are
caused by the presence in the latter case of bicarbonate and carbonate
species from the dissolution of the calcium carbonate.  These species
affect the pH and buffering capacity of the basic aluminum sulfate
solution.

     The flat portion of the pH curve is the region of interest in the
application of basic aluminum sulfate as a scrubbing reagent.  For
scrubber applications the range of compositions is limited to (NQH/NAI)
values of about 0.3 to 1.2, where  (NQR/NA!) is the ratio of moles of
hydroxide ion per mole of aluminum ion present.  The lower limit is
chosen to prevent completely exhausting the scrubbing capacity of the
liquor, and the upper limit is chosen to prevent potential precipitation
of aluminum from the liquor, which would lead to the loss of the aluminum
in the gypsum end product produced in the process.

     Within the composition range of interest, the liquor pH only changes
by 0.2 to 0.5 pH units.  This small pH change precludes the use of pH as
a process control mechanism.  Therefore, in the Dowa process, process
control is based upon liquor composition using basicity, B, which is
defined as follows:
                          B
     As examples of the concept of basicity, consider the following:

                       Compound         Basicity  (%)

                                             0
                    Al(OH)"t'(3~x)           IQOx
                          x                  3

                    A1(OH)3                100


     Three independent means of determining  liquor basicity  can be used
 in process control.  The liquor basicity is  monitored by an  in-line
 basicity analyzer which determines the liquor basicity automatically on a
 continuous basis.  In addition, the liquor basicity can be determined by
 direct titration in the laboratory or calculated  from the results of an
 analysis of a lj>—»r sample.
                                     315

-------
co
M
en
I I




10




 9




 8




 7




 6




 5




 4




 3




 2




 I
                             I     I     I    T
                                           i    \     r     i
                                                                                i     i
                    I
                         A-20  ml  O.IOM AI2(S04>3 with  O.I  N HCI and 0.1  N  NaOH as titrants




                         B-IOO ml O.IOM AI2CS04>3 titrated  with 3.45g of CaC03
                                                	I
I
I
   2.8 2.4  2.0  1.6  1.2 0.8  0.4   0  0.4 0.8  1.2  1.6 2.0 2.4  2.8  3.2  3.6 4.0  4.4



                                      0       25       50       75       100
                                                             25       50      75

                                                                  Basicity <%)
             Figure  1.   Relationship of pH to basicity and ratios of mols of  OH  and H  to mol of Al

                         during acid and base titrations of A]_2 (80^)3 solutions.

-------
SHAWNEE DOWA PROCESS EQUIPMENT DESCRIPTION

     Figure 2 is a flow diagram of the Shawnee train 200 after installation
of process  equipment.  The aluminum recovery step was not included in
the process demonstration due to limited funds.  The major process
equipment utilized included:

 1.  The existing TCA scrubber complete with nitrile foam spheres and
     a single absorber hold tank (spheres were replaced with rigid
     packing during the test program)

 2.  An air sparger system, including a blower and pipe sparger located
     near the bottom of the absorber hold tank

 3.  Two neutralization tanks installed in series

 4.  An existing thickener utilized for initial gypsum dewatering

 5.  An existing horizontal-belt vacuum filter for final gypsum dewatering

 6.  A reclaimed absorbent hold tank

 7.  An aluminum sulfate solution preparation and feed system

 8.  All process pumps and agitators associated with the above equipment

     Sulfur dioxide absorption occurs in the TCA absorber.  The oxidation
process step occurs in both the absorber and the absorber hold tank.  A
bleedstream of absorbent is pumped to the neutralizer tanks, where the
limestone required for neutralization is added.  The neutralizer product
overflows from the second neutralizer into a conventional thickener.
The thickener overflow is collected in the reclaimed absorbent tank, and
the thickener underflow is pumped to the filter for final dewatering of
the gypsum byproduct.  The filtrate is returned to the reclaimed absorbent
tank.  A portion of the thickener underflow is recycled to the first
neutralization tank to provide gypsum seed crystals for the neutralization/
gypsum precipitation step.

     The basicity of the absorbent in the absorber loop and the reclaimed
absorbent is continuously monitored with an automatic basicity analyzer
and routinely analyzed in the test facility laboratory.  The basicity of
the reclaimed absorbent is controlled by varying the limestone feedrate
to the neutralizer tanks.  The basicity of the liquor in the absorber
loop is controlled by varying the rate of the absorbent purge to the
neutralization section.

     The aluminum concentration in the absorbent is monitored by laboratory
analysis and controlled by aluminum sulfate solution addition to the
absorber hold tank.
                                     317

-------
                            TO REHEATER
00
l->
00
                                                                                                      LIMESTONE SLURRY

                                                                                                         HOLD TANK
                                                 ALUMINUM SULFATE

                                                   MAKE-UP TANK
                              ABSORBER LIQUOR

                                 HOLD TANK
                                                                                        PURGE
RECLAIMED ABSORBENT

       TANK
                  Figure 2.   Dowa  process  demonstration flow diagram.

-------
TEST RESULTS

     Construction of process equipment changes for the Dowa demonstration
was completed in November 1979.  Following the completion of construction,
numerous equipment-related startup problems plus boiler outages prevented
continuous operation of the process demonstration until January 1980.

     The major operating conditions selected for the 1-month demonstration
are summarized in Table 1.  Problems continued to hinder stable continuous
operation during the 1-month demonstration.


                   TABLE  1.  DOWA PROCESS DEMONSTRATION

                   SELECTED ABSORBER OPERATING CONDITIONS
                      Operating condition
            Inlet flue gas rate, aft^/min at SOO'F     25,000
            Inlet flue gas fly ash loading, gr/sft3     'V-O.IO
            TCA sphere bed static height, inches
              Bed 1                                         5
              Bed 2                                         5
              Bed 3                                         3
            Basicity, %
              Absorber loop                                10
              Reclaimed absorbent                          27
            Aluminum concentration, g/&                    20
            Absorber recycle rate, gal/min              1,250
            L/G, gal/kft5                                  58
            Oxidation air stoichiometry,
             Ib-atoms 0/lb-mol  S02 absorbed               4.0
     These problems included:

 1.  Freezing and plugging the basicity analyzer sample lines caused
     by poor location of the sample lines and the failure of heat trace
     material.

 2.  Unstable standard solutions for calibration of the basicity analyzer
     caused the process to be controlled either above or below the
     desired basicity set points.  (This problem was not resolved until
     near the end of the demonstration and may be responsible for scattered
     test data.)

 3.  The method for determination of dissolved sulfite in the scrubber
     liquor was inaccurate.  (This problem was solved by addition of
     iodine to samples to  stabilize the sulfite concentration prior to
     analysis and elimination of the filtration step in the analytical
     procedure.)
                                    319

-------
 4.  Following the initial startup, inspection of the TCA  absorber walls
     and absorber spray nozzles revealed that calcium sulfate  scale
     deposits (from previous limestone scrubbing tests in  the  TCA) were
     dissolving in the Dowa liquor, breaking loose from the scrubber
     internals, and plugging the absorber spray nozzles.   Testing was
     delayed while scale was manually removed from the absorber internals.

     Despite the resolution of the above stated problems,  SCL  removal
efficiency still did not match the design expectations.  In lieu of the
continuing process demonstration, a series of TCA screening tests to
determine the S02 removal efficiency of this absorber over a wide range
of flue gas rates, absorbent recirculation rates, and oxidation air
flowrates were performed.  Attempts to improve control of  basicity and
oxidation continued during these tests.  The.862 removal efficiency of
these tests continued to be lower than expected from the Dowa  process
operating with a TCA scrubber in Japan.  The TCA static sphere bed depth
was increased to 8 inches with little effect on SC>2 removal.   The maximum
sustained SC>2 removal during this test was 87%.  Observation of the
sphere action during absorber operation and. sphere distribution in the
beds after the absorber shutdown indicated that the gas distribution in
the TCA was poor.  Consequently, poor gas/liquor contact was suspected
to be the cause of the low removal efficiency.

     The nitrile foam spheres were replaced with fixed-bed packing, and
the remainder of the test program was dedicated to absorption  studies
with this type of packing.  Three series of tests were conducted:  two
series with a 9-foot packing height, and a third with a 6-foot packing
height.  The ranges of major operating conditions during these tests
included:

  Flue gas rate, aft3/min at 300°F      13,000-27,000 (low fly ash loading)
  Superficial gas velocity, ft/sec         5.4-11.2
  Recirculated absorbent, gal/min          700-1,400
  L/G, gal/kft3                             39-126
  Absorber AP, in. H20                     1.0-14.7
  Absorbent basicity (absorber), %        11.0-35.2

     The fixed-bed packing approaches flooding conditions  when the absorber
is operated at 27,000 aft3/min (equivalent to 10 MW and an absorber super-
ficial gas velocity of 12 ft/sec).  S02 removal efficiency did not remain
above 90% and steady operation was therefore not possible  at a gas rate
equivalent to 10 MW.

     After the superficial gas velocity was lowered to between 6 and 9
ft/sec, more stable operation and high S02 removal efficiency were
achieved.   For example,  90% to 97% S02 removal was achieved while the
absorber operating conditions were 20,000 aft3/min flue gas rate, L/G
equal to 55, and pressure drop equal to 9.2 to 10.5 inches H20; 93% S02
removal was achieved while the absorber operating conditions were 20,000
aft /min flue gas rate,  L/G equal to 82 gal/kft3, and pressure drop
equal to 9 inches of water; and 93% to 97% S02 removal was achieved while
the absorber operating conditions were 13,000 aft3/min flue gas rate, L/G
equal to 90 to 125 gal/kft3,  and pressure drop equal to 1.5 to 2.5 inches
H2°r

                                     320

-------
     During the tests with 6 feet and 9 feet of packing in the absorber,
an excessive oxidation air stoichiometry was maintained to assure near
complete oxidation of the absorber liquor and to enhance S02 removal in
the absorber.   The sulfite concentration in the recirculated absorber
liquor during the tests was ^0 to 60 mg/£.  Data collected during the 6-
foot fixed-bed packing tests are plotted in Figures 3,  4, and 5.   Data
collected with 9 feet of packing are being evaluated and will appear in
the Dowa project final report.

     A typical gypsum byproduct composition during the  absorption factorial
tests is as follows:

                	Component	% by wt (dry)

                Aluminum                       0. 3a
                Calcium                       21.8
                Carbonate                      Nil
                Sulfite                       JfcO.O
                Sulfate                       53.8
                Total solids  (wet basis)      81.8
                Acid insolubles                Nil
                a.  Gypsum cake washing procedures
                    were not optimized.  Lower aluminum
                    concentration is expected with im-
                    proved cake washing, such as 0.05%
                    Al achieved in commercial facilities
                    in Japan.

     The final test was performed with flue gas taken from the duct
before the precipitator and thus the gas to the absorber contained full
fly ash loading, %A.O gr/aft^.  No significant effect by the fly ash
upon the process was observed during this 1-week test.
SUMMARY OF RESULTS

     The results of the Dowa test program are summarized as follows:

  •  Difficulties which were encountered during the Shawnee tests, such
     as problems with analytical procedures for sulfite and preparation of
     stable standard solutions for the basicity analyzer calibration,
     undoubtedly had an adverse effect upon the removal efficiency of S02«
     Also, the apparent poor gas distribution in the Shawnee TCA adversely
     affected the test results.  Although the Dowa process did not effec-
     tively remove 90% of the S02 in the flue gas from a coal-fired boiler
     while operating with a mobile-bed scrubber, the quantitative effect
     of each of these problems upon the observed S02 removal efficiency
     of the TCA is unknown.
                                     321

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 fiC
 G
 O
 Z
 UJ

 o
 SI
 uu
  Hi
  CC
 O
      95
90
85
80
      75
70
      65
      60
                 5.0    6.7    8.3   10.0   11,7   13.3


               SATURATED GAS VELOCITY, FPS



Figure 3.  Mass transfer characteristics:  Polygrid packing - six foot data.
                             322

-------
o
z


o

Q.

H
LL

d
  •
£
Q.
O
cc
c
CO
UJ
^
Q.
      4.0
      3.5
      3.0
      2.5
      2.0
      1.5
      1.0  }-
      0.5  *-
                                             13CO
                 5.0    6.7     8.3   10.0   11.7   13.3


                  SATURATED  GAS  VELOCITY, FPS


Figure 4.  Absorber pressure drop:  Polygrid packing - six foot data.
                              323

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#   95
>
K
a
 *   90

o
     85
UL
IL
IU
     80
     75
Ut
ee
 w  70

O
CO


     65
     60
                I   I
      TESTING RANGE


GAS:  13,000-27,000 SCFM

  LIQUID: 600-1300 GPM
I    I
I    I
                                 I
          I
                50                 100                150


            LIQUID  TO  GAS  RATIO,  GAL/MSCFM



Figure 5.  SC>2 removal  efficiency versus liquid to gas ratio:
         Polygrid packing - six foot data.
                           324

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 •  The SOp removal efficiency  of  the  process  is  improved  to  greater
    than 90% by providing better flue  gas  and  absorbent  contact with a
    fixed-bed packed  absorber.  For  example, with 6  feet of rigid
    packing in the absorber,  93% S02 removal is achieved while operating
    at 9 ft/sec superficial  gas velocity,  .82 gal/kft3  L/G, and 9 inches
    H20 scrubber  pressure drop.

 •  The neutralization and dewatering  steps; of the process can effec-
    tively produce a  gypsum  byproduct.

 •  High concentrations of fly  ash in  the  process absorbent do not
    affect the process performance (a  preliminary result from a 1-week
    test).

 •  There is no scale formation in the absorber.
CURRENT AND FUTURE TESTS

     UOP is now performing laboratory studies and installing an integrated
pilot plant to further optimize the Dowa process.  TVA and UOP have
independently proposed further Dowa process tests at Shawnee.   These
further tests at Shawnee are contingent on completion of these laboratory
and pilot tests and an economic evaluation of the process.
                                    325

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                           F.G.D. EXPERIENCES


                            SOUTHWEST UNIT 1


          N. Dale Hicks, City Utilities, Springfield, Missouri


            O. W. Hargrove, Radian Corporation., Austin, Texas


                                ABSTRACT
     City Utilities of Springfield, Missouri, began commercial operation
of this F.G.D. system in September, 1977.  Two turbulent contact absorber
modules are arranged in parallel and utilize a pulverized limestone slurry
for S02 removal.  The scrubbers serve a 195 M.W. unit with a Riley Stoker
boiler burning 3.5% sulfur coal.  Station design was by Burns & McDonnell,
with the Air Correction Division of Universal Oil Products, Inc. responsible
for the F.G.D. system on this new facility.

     The absorber modules and various support systems have experienced a
variety of problems since initial start-up.  The more severe problems
encountered have been:  absorber and demister pluggage; failure of absorber
spheres; pipe breakage; control and instrumentation malfunctions; and
expansion joint, damper, and duct corrosion.  Past and planned efforts
to rectify these difficulties, and to improve F.G.D. system reliability,
are discussed in detail.

     A related problem area has been the continuous monitoring systems
for flue gas opacity and SO2 emissions.  Original equipment has proven
unsuccessful and the investigation toward a solution, with the aid of a
consulting firm, is described.

     The station is to be the host facility for an E.P.A. sponsored full
scale demonstration of adipic acid as an additive to wet limestone F.G.D.
systems.  Anticipated results are enchanced efficiency and improved
operation of the pollution control facility.  Also involved in the project
is the Radian Corporation and Universal Oil Products, Inc.
  Preceding page blank
                                     327

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                             FGD EXPERIENCES

                            SOUTHWEST UNIT 1
     Southwest Unit 1 is a 194 MW fossil fueled unit owned  and  operated
by City Utilities of Springfield, Missouri.  The unit was designed by
Burns & McDonnell.  Commercial operation, of the generating  unit began
in May, 1976 while the FGD Systems were not fully operational until
September 1977.

     The steam generator was supplied by Riley Stoker Corporation  and was
designed to burn high (3.5 to 4.0 percent) sulfur coal.  Air Correction
Division of Universal Oil Products (UOP) furnished and installed the
electrostatic precipitator and the two-module flue-gas scrubber.   Each
absorber module consists of a presaturator area; three TCA  beds, each
containing spheres to enhance gas-liquid mixing; two chevron mist  eliminator
banks; and a reaction hold tank.  A common limestone preparation area and
sludge dewatering train serve both modules.  The design was based  on a
limestone composition of 98.7 percent CaC03, 0.7 percent MgCO3/ and 0.6
percent inerts.

     The attached Figure 1 presents the process flow diagram.   Basically,
the induced draft (.ID) fans pull the flue gas from the boiler through the
air heaters and the electrostatic precipitator (ESP) and discharge into
the scrubber inlets.  Particulates (fly ash) are removed from the  flue gas
by the ESP and conveyed to dry storage.  SO_ removal is attained in the
scrubber with waste products of the reaction removed by continuous outflow
from the scrubbers to a thickener tank.  The thickener separates the water
(supernatant) from the waste solids and recycles the water  to the  scrubber
system.  The waste solids are drawn from the thickener and  passed  across
a travelling vacuum belt for further removal of water.  This sixty to seventy
percent solids waste is then mixed with dry fly ash to produce  a fixed
material which is landfilled on site.

     Limestone is prepared for the scrubbing process by wet grinding in two
(2) ball-tube mills.  There is no classification of the ballmill outputs so
fineness of grind cannot be readily controlled.

PROBLEM AREAS

     Numerous problems have plagued the FGD systems at Southwest Unit 1.
Some problems have been solved, others are still being dealt with.  The
following sections will detail the major classifications of problems
experienced and findings relative to their evaluations.

Pluggage

     Pluggage in both the demister sections and the absorption  areas of the
scrubbers originally hampered reliable operation of the FGD system.  During
initial start-up and shakedown of the scrubbers it became readily  apparent
that the demister wash system was inadequate.  The system was designed to
operate as a closed loop as shown in Figure 2.  Within two  weeks of only
partial operation the demister chevrons were thickly scaled.  Continuous
recirculation of the solids-ladened wash water caused a further scrubbing
action in the demister area resulting in scale formation and serious plugging.

                                     328

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                        ELECTROSTATIC
                         PRECIPITATOR
co
N>
UD
  AIR
HEATER
                                               'B'l.D.
                                               FAN
                                               'A'l.D.
                                               FAN
                                                               LIMESTONE
                                                                 SLURRY
                                                                   1   'B'ABSORBER
                                                                 ^-J-^  MODULE
                                                              Hi
                                                                      \
                                                                      T
                                                                     SLUDGE
BYPASS DUCT

    LIMESTONE
      SLURRY
                                                                      Y
                                                                      r
                                                                     SLUDGE
                                                                       'A'ABSORBER
                                                                         MODULE
                                                                                                      STACK
                                                                                               70-1910-1
                                   Figure 1     Southwest Unit 1 Process Flow Diagram.

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OJ
o
                                                                                                FROM
                                                                                              DRAW-OFF
                                                                                                SUMP
                                                                                         SUPERNATANT
                                                                                            TANK
                                              MIST
                                           ELIMINATOR
                                           WASH TANK
                                                                                            LIMESTONE
                                                                                 RECYCLE
                                                                                  PUMPS
                                                   TO
                                               THICKENER
FILTER CAKE
(MIXED WITH
FLY ASH FOR
 LANDFILL
 DISPOSAL
                                                                                                                        701911-1
                                                  Figure 2    Southwest Unit 1 Scrubber Flow Schematic.

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     This  situation was improved by a redesign of the demister spray and
presaturator spray systems as shown in Figure 3.  Instead of a closed loop
system,  the demister spray system was changed to utilize supernatant water
in a once-through flow sequence.  This water was then collected and repumped
to provide the source for the presaturator spray system, and to wash the
underside  of the trap-out-trays.

     This  modification has improved the operability with regard to the
demisters.  Pluggage and scaling occurs much less frequently, but improve-
ments are  still being sought by plant personnel.

     Absorption area pluggage can be traced in part to the following factors:
sphere failure, inadequate limestone grinding, and on-off-on cycling.
Sphere failure has been a problem since the original system start-up.  The
original sphere supplied by UOP was a seven gram white  (TPR) sphere similar
in appearance to a ping-pong ball.  The spheres were installed in only one
layer per  module initially.  Two levels per module were added prior to the
September, 1977 acceptance testing.  It was evident after only a few weeks
of continuous operation that the spheres were failing.  Many ruptured and
filled with slurry; others collapsed or dimpled losing their buoyancy.  The
sphere layers were no longer completely fluidized and behaved as solids
filters resulting in severe absorber pluggage.

     A random sampling of the spheres was conducted in September, 1978, to
determine  the failure rate of the TPR spheres.  It was determined that
virtually  all of the spheres had either totally failed or were badly deform-
ed.  Following discussions with UOP it was decided to replace the TPR
spheres with black foamed nitrile rubber spheres (eleven grams each).  This
replacement was made in October, 1978, with a bed thickness of approximately
8 inches as prescribed.  Upon scrubber start-up after this sphere replace-
ment, a significant increase in pressure drop through the scrubbers was
detected.   Only about ninety percent of full load could be reached because
of the inability of the I.D. fans to make up the additional pressure drop.
Additionally the spheres began absorbing moisture, thus reducing their
buoyancy and creating the same type of pluggage problem that had existed
with the damaged TPR spheres.

     In an effort to solve this situation, the sphere bed depths were
reduced from 8 inches per layer to approximately four inches per layer.
Some increase in load carrying capability was realized for short periods of
time, but  the failure rate of the spheres was still rapid.  Many split in
two; others shriveled and cracked and lost their buoyancy.  Weekly cleaning
of the ball cages was sometimes not sufficient to prevent complete pluggage
of the sphere layers.  It was not uncommon for plant employees to dig spheres
out of the pluggage with screwdrivers in attempts to clear the residue from
the cages.

     In early 1980, it was decided to evaluate other spheres for possible
replacement.  A sphere, manufactured by Puget Sound Trading Co., was select-
ed for testing.  These spheres are green in color and approximately the same
size and weight as the original TPR spheres, but with cast ridges for addition-
al structrual strength.  The spheres were installed during the summer of
                                     331

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                              MAKEUP
                              WATER
                                                                                        FROM
                                                                                      DRAW-OFFlr-
                                                                                        TANK
                        MIST
                      ELIMINATOR
                      WASH TANK
                     PRESATURATOR
                         TANK
Co
co
ro
                                                          ABSORBER
                                                            STAGES
                           PRESATURATOR
                           TANK OVERFLOW

                                 HOLDTANK
                                 OVERFLOW
SLURRY
MAKEUP
                                                  HOLDTANK
                                                                                  SUPERNATANT
                                                                                      TANK
                                                                                     LIMESTONE
FILTER CAKE
(MIXED WITH
FLY ASH FOR
 LANDFILL
 DISPOSAL)
                                            70 1912-1
                                                                     RECYCLE
                                                                     PUMPS
                                               TO
                                           THICKENER
                                               Figure 3    Southwest Unit 1 Scrubber Flow Schematic.
                                                                  Revised 5-77

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1980  and  to  date no substantial pluggage problems have been encountered.
Unit  load-carrying ability has returned to original design levels.

     City Utilities is currently evaluating the conversion of the scrubbers
from  fluidized bed contacting to a tray type design.  This conversion has
been  completed at other locations and appears to have improved both the
economics and the availability of the scrubbers.

     Funds to provide and install limestone classification equipment follow-
ing the ball mills have been budgeted.  When this equipment is installed and
put into  service, it is anticipated that limestone utilization will improve
and pluggage frequency decline.

Expansion Joints

     The  I.D. fan outlet expansion joints have been a source of considerable
scrubber  downtime and expense.  The joints originally installed by UOP
were  manufactured of high-strength low-alloy steel.  Within a few months of
operation, it was evident that the joints were failing.  During the fall
1977  outage, the steel expansion joints were replaced by UOP with Viton
rubber joints.  During 1978, over 3,000 hours of scrubber module downtime
resulted  from numerous failures of these expansion joints.

     In early 1979, plant maintenance personnel accepted the responsibility
of maintaining the joints from UOP.  Joint life at that time could be
expected  to range from two hours to two or three weeks.  An analysis of
samples taken from failed joint specimens indicated an internal abrasion
failure mode.  The presence of hardened fly ash and limestone in the insul-
ation boot on the flue gas side of the rubber Was determined to be the source
of the abrasion.

     Further evaluation into the presence of the calcium material indicated
that the  probable cause was presaturator spray nozzle pluggage.  With a
nozzle plugged, flow of the spray could be directed into the duct counter
to the flow of the flue gas stream.

     In May, 1979, the expansion joint was redesigned.  The Viton material
was placed on the inside of the joint in contact with the flue gas.  A
neoprene  belting material was utilized for an external cover with insulation
fill  between the two layers.  Additionally, a small plate was installed
across the floor of the ductwork downstream of the expansion joint to halt
errant presaturator spray.

     Since these modifications in mid-1979, the life expectancy of these
expansion joints has increased to at least six months.  It is anticipated
that  with slightly thicker belting material longer joint life can be achieved.
The evaluation of expansion joint performance is. ongoing.
                                     333

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Piping

     Most of the scrubber piping systems at' this  installation are made  of
fiber reinforced plastic  (FKP) pipe.  The pipe, manufactured  by Fibercast
Co.  (Div. of Youngstown Sheet & Tube Co.) and installed by  OOP is resistant
to abrasive wear.

     The Southwest Unit 1 Scrubber installation is not enclosed;  i.e.,  all
piping systems are exposed to ambient weather conditions.   The first winter
of scrubber operation demonstrated the vulnerability of FRP pipe to cold
weather failure.  There were three types of failures:  failure due to
freezing; failure due to pipe embrittlement; and  failure of the joint
adhesive.  Proper heat tracing and insulation of  an FRP piping system is
most difficult because of its poor conductivity.  There were  instances  of
FRP pipes with heat tracing and insulation that froze during  the  winter of
1978-79.

     After evaluating various repair possibilities of the FRP piping systems
and researching other piping options, it was decided during the summer  of
1979 to replace the mist eliminator trap-out-tray piping system with a  lined
steel pipe system, manufactured by Peabody Dore.  This replacement was
accomplished in October, 1979.  The new piping system was heat-traced and
insulated in a proper manner.  This piping system, historically the most
susceptible to freezing, did not sustain a single failure during the 1979-80
winter period.

     Because of the improvements noted in the new piping system,  it is
planned to replace all FRP scrubber piping with a lined-steel piping system
in the fall of 1980.  With proper heat-tracing and insulation,  pipe freezing
and breakage problems should be greatly reduced.

Corrosion

     As with most scrubber installations, corrosion causes  continuing and
extensive maintenance.  Corrosion has caused deterioration  of dampers,  seal
strips, ducts, linings, and exposed metal surfaces in the outplant area.

     Very shortly after initial scrubber start-up it became apparent that
material selections were not what they should have been.  The chloride
concentration in the scrubber slurry has been measured as high as  2000  to
3000 ppm.  Entrained mist that was not removed by the demisters collected in
the outlet duct, exposing the dampers, seal strips, and lining materials to
the high chloride liquid.  In addition, continued contact of  the  liquid with
the flue gas resulted in a lowering of its pH to  between 1.0  and  1.5 due to
further S02 absorption.  The combination of this  high chloride low pH
environment resulted in severe corrosion and rapid material deterioration.
The original outlet duct lining, Rigiflake 485, began peeling approximately
two weeks after initial scrubber start-up in April, 1977.   Attempts were
made to spot-patch the failed liner areas.  In October, 1977  the  entire.
outlet duct surface was cleaned and relined again with Rigiflake.  Within
a month of operation,  the liner had again failed.
                                     334

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     Evaluations by the owner and OOP representatives led to the selection
of a different liner material for installation during a planned outage in
October, 1978.  Two variations of the liner material, Placite 4005 and
Placite 4030, were used.  After being in service for approximately one month,
the duct liners were inspected and found to be in very good condition.
After the second month of service, deterioration of the liner was quite
advanced.  In April, 1979, the Placite application contractor returned to the
site to patch the failed areas and any other areas that were deteriorated.

     After a few months of service, liner failure was again apparent.  The
failure appearance was in most cases that of a blister.  The Placite would
separate from the metal duct allowing corrosion of the metal beneath the
Placite.  It was determined that improper metal surface preparation was
the probable cause of the failures.

     During the month of October, 1979, the ducts were sandblasted to white
metal, and relined with Placite.  During the process, all deteriorated
metal areas were patched and turning vanes replaced.  Within three months
of operation, the Placite lining had deteriorated sufficiently in certain
areas to allow holes to be eaten through the one-quarter inch A-36 steel
duct material.

     At this time other liner materials are being evaluated.  Hastelloy
G (Cabot) appears to be a prospect for use but is so expensive that the
budget will not allow its use.  Resista-Flake by Corrosioneering has some
applications which seem to have served marginally well.  At the time of
this writing, no final decision had been made as to the material to be
selected for duct liner repairs in the fall of 1980.

     Some gains have been made in the selection of materials for dampers
and seal strips.  The original scrubber inlet and bypass damper seals were
of 304L stainless steel; the frames and blades were of A36 steel.  Within
one month of operation, failure was evident.  UOP then replaced the seals
with 316L stainless, the same material as the outlet dampers.

     By the fall fo 1977 it was evident that the 316L material was not
suitable for the pH and chlorides present.  UOP replaced the inlet and
bypass damper seals and the outlet dampers in December, 1977.  The inlet
and bypass damper seal material used was Inconel 625 Huntington Alloy;
the outlet damper material used was Udeholm 904L, including seal strips.

     To date, the Udeholm 904L outlet dampers have provided good service.
Some slight seal strip deterioration is evident and will be corrected.
The Inconel 625 inlet and bypass damper seals have not performed as well.
The seal strips have been completely corroded away and the carbon blades
and framework are badly deteriorated.  An evaluation of materials to
replace these dampers is underway at the time of this writing.

     The originally installed presaturator lining, Precrete Grout,
began failing soon after its application and before the scrubbers were
placed in service.   Severe cracking appeared as if it were shrinkage induced.
The installation contractor made repairs on two different occasions in
an attempt to save the liner but to no avail.  By late summer, 1977, holes
were eaten through the outer wall of the duct.
                                     335

-------
     During the outage that began  in  September  of 1977,  UOP removed the
Precrete material and relined the  entire presaturator area of the scrubbers
with Udeholm 904L.  This material  served appreciably better than the Precrete.
The Udeholm lining required no maintenance  until  October,  1979,  when several
sections had to be patched.  Some  degree of deterioration  was evident over
most of the Udeholm lining indicating that  a more resistant material was
needed.  All repairs utilized Hastalloy G material in the  presaturator area.

     An inspection was conducted of the presaturator area  during April, 1980.
Further deterioration of the Udeholm  lining was evident.   Several materials
were considered for repairs.  Laboratory testing  of Plastaloy (by Continent-
al Alloy Steel) indicated it possessed high abrasion resistance  and high
corrosion resistance.  It was decided to try some of this  material in one
scrubber module.  The sheets of the material were installed using special
nylon bolts.  The material lasted  less than one week in  operation.  Apparent-
ly the expansion of the material differed substantially  from the metal caus-
ing the Plastaloy to twist and wrench its way apart from the duct.
Investigation is continuing into materials  for  future use  in this area.

Instrumentation

     Many of the problems initially encountered in the instrumentation
area were caused by long periods of inactivity  while UOP performed needed
modifications on the FGD Systems.  When UOP left  the job site City Utilities
found itself without an adequately trained  technical force to trouble-shoot
and maintain the systems.  The maintenance  staff  has been  expanded and train-
ing provided so that we now have good capabilities to deal with  instrumenta-
tion and control problems.

     Freezing problems have beset many of the instrument systems since the
first winter of operation.  Instrument air  drying capacity,  as originally
installed, was sorely inadequate.  The passage  of this inadequately dried
air through small-diameter air control lines caused condensation in the
air lines and eventual freezing.  Damage to transmitters and various other
instrumentation resulted.  From initial scrubber  operation until February,
1979, some 1500 hours of module downtime had occurred because of icing in
air lines and instrumentation.

     A new instrument air dryer installation was  funded by City  Utilities
and the installation completed in February  1979.   This dryer unit was of the
dessicant type and has served well.   During the spring and summer of 1979,
the air lines and instruments were cleaned  and  purged to insure  that no
moisture remained in the lines.  As a result, there were no instrument air
line freezing problems during the winter of 1979-80.   One  plant  air line
which supplies air to the limestone ball mill clutch control did freeze
last winter.   A dessicant dryer assembly will soon be added to that air
system to correct the situation.

     Another instrument freezing problem which  has caused  considerable
difficulty and module downtime is the pH monitoring system.   Each scrubber
module has an on-line pH analyzing system with  two glass electrode sensors.
The sensors are located in a small open tank through which the slurry flows
continuously.   During extremely cold  weather, ice forms around the sensors
                                     336

-------
usually resulting in breakage of the sensors.  Pluggage of the sensors by a
build-up of slurry requires frequent cleaning which eliminates the possible
use of a full enclosure.  New in-line pH cells are now on order.

     Continuous monitoring of flue gas opacity and SO  has been totally
unsuccessful.  The original opacity monitors were Lear Sielger RM-4 instru-
ments which were installed in the. I.D. fan outlet ducts.  They never operated
reliably and failed soon after installation.  The static pressure in the
duct where they were installed could easily reach 20 inches  (W.C.).  The
purge air fans on the instruments were inadequately sized to cope with this
pressure, thus making cleaning and other maintenance of the monitoring equip-
ment difficult because of flue gas infiltration.  Corrosion of the equipment
eventually rendered it useless.

     The original flue gas S02 monitoring equipment was a model 1268-2-21
Turnkey Gas Analysis System installed by Dynasciences Inc.  This was an
extractive system with the sample obtained from the wet gas stream at an
upper stack platform (255 feet above ground level).  The sample line, heat
traced and insulated, ran from this sample point down to the ground, then
to the scrubber control room where the monitoring equipment was located.
The total length of this sample line was over 400 feet.  During operation,
sample line pluggage was nearly a daily occurence.  If the sample probe
plugged, a technician was required to climb the stack ladder to the sample
probe level to clean and repair the probe.  This was quite an unpopular duty,
and during wet or freezing weather was unsafe.

     After discussions with various vendors, and continued lack of success
with further equipment modifications, it was determined that the existing
systems were not capable of operating in a reliable manner.

     City Utilities evaluated consultants that specialized in the field of
flue gas monitoring and testing and selected Entropy Environmentalists, Inc.
to study the problems of the existing installations and to evaluate modifi--  .
cations or redesign of the monitoring equipment installation.  Some of this
work has now been completed.  A new, low pressure zone location has been
tentatively selected for the opacity monitors.  The monitors would in fact
be located at the I.D. fan inlets in a negative pressure zone.  The flue
gas S02 sampling point will be relocated to a lower stack platform just
above the scrubber outlet duct.  A stairway is planned to connect the scrubber
to this platform and eliminate the need to climb the stack ladder to service
the equipment.

     The specific equipment to be used is still being evaluated.  Perfor-
mance specifications have been prepared.  Entropy is not presently aware of
any monitoring equipment vendor who has successfully installed a system on
a wet stack which operated as reliably as required by the involved govern-
mental agencies.  Few,  if any vendors are willing to warranty their equip-
ment installation for any period of time after an acceptance test and their
people leave the site.   Our experience has been that a vendor's serviceman
can get his equipment in. operation,  leave the site, and his equipment would
again be inoperative before he would reach the airport.
                                     337

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 Thickener/Dewatering Systems

      The waste slurry enters  the  thickener  from the scrubbers with betweer
 five  and fifteen percent by weight  solids content.   Solids settling in the
 thickener is aided by the addition  of polymer.   Frequent sampling of the
 mixture to determine the settling rate  is required  to maintain proper inter-
 face  levels.  The solids in the slurry  must not settle out to more than
 thirty to forty percent by weight or pluggage of lines and pumps occurs.
 If  the solids stay in suspension  they overflow the  thickener and are return-
 ed  as supernatant to the scrubber.  These returned  solids can contribute to
 pluggage of demister nozzles.

      One problem encountered  in the thickener tank  has been anaerobic
 bacterial attack on sulfites  and  sulfates resulting in a change of color
 of  slurry and cake from cream to  gray with  a resultant smell of rotten eggs
 (H  S  formation) .  This problem occurs during warm weather and when the slurry
 is  retained in the thickener  during breakdowns  on the system lasting longer
 than  a day.  The bacteria have been controlled by "shocking" the thickener
 tank  contents with swimming pool  grade  granular chlorine (usually four-hund-
 red to five-hundred pounds broadcast into the thickener tank that has 750,000
 gallons capacity).

      The under flow from the  thickener  is pumped to an EIMCO Vacuum Filter
 belt  and discharged to conveyors  with sixty to  seventy percent solids.   A
 conveyor transports the dewatered sludge to a pug mill where it is mixed
 50/50 (by weight) with dry fly ash.  This produces  a material which is
 directly landfilled.  During  freezing weather,  spillage of the material
 causes pluggage and freezing  of the conveyor tracks.   Torn conveyor belts,
 which results in temporary shutdown of  the  system,  have been common.
 Complete enclosure of this process  has  been comtemplated but funds have
 not been available to accomplish  the work.

      A limiting factor in the dewatering operation  is the pug mill.   Its
 capacity is such that at continuous high operating  levels,  sixteen to twenty
 hours of operation per day are required to  maintain the solids level within
 the thickener tank at an acceptable level.

      There is no redundancy of conveyors or the pug mill.   If one breaks,
 the system is down and the draw-off from the thickener must either be pumped
 to  the emergency pond or discharged to  the  ash  pond.   This  type of break-
 down would not immediately affect the operation of  the scrubbers.

 Other

Beneath each scrubber module in the hold tank is a  large turbine agita-
 tor manufactured by Lightnin Co.  The drive shaft for the agitator is approx-
 imately twenty-two feet (22')  in  length and is  six  inches (6")  in diameter.
 The shaft in the "B" scrubber module has now fractured twice.   The first
break occurred in May,  1979.  An  analysis of the break indicated frequency
related flexural fatigue failure.  While awaiting replacement material,  the
                                     338

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design of the hold tank and agitator shaft was evaluated to determine the
cause of flexure in the shaft.  No conclusive determination was made so a
new shaft was installed and the scrubber returned to service in July, 1979.
This new shaft failed in May, 1980.  This failure differed from the initial
one in that it occurred at a factory weld and there was no indication of
fatigue.   A new shaft was fabricated locally and the scrubber returned to
service.   The cause of this failure is still being diagnosed by the manufac-
turer.

     Consideration has been given to two other additions which would undoubt-
edly improve overall scrubber availability.  They are:

     a)  a spare (3rd) scrubber module
     b)  freeze-proof the FGD systems by totally enclosing them.

The cost of providing these improvements have prohibited serious considera-
tion of them.

ADIPIC ACID TEST PROGRAM

     City Utilities is a progressive organization and is interested in
improving its operation.  When it was learned that the Environmental Protection
Agency (EPA)  was proposing to sponsor a full scale demonstration of adipic
acid addition to limestone scrubber operations, management was interested.

     A contract now exists between Radian Corporation and EPA for this
demonstration program.  City Utilities is providing the host site (Southwest
Power Station Unit No. 1) and other support services.  The Air Correction
Division (ACD) of UOP is also participating in the program.

     The addition of weak organic acids such as adipic acid to limestone FGD
systems has been shown to benefit both SC>2 removal and limestone utilization
and, also, to have a potential for improving the overall operability of a
limestone FGD system.  Adipic acid has the effect of buffering scrubber
solutions, thereby enhancing liquid phase mass transfer.  EPA has tested
adipic acid addition to limestone scrubbers at a 0.1 MW pilot plant in
Research Triangle Park, North Carolina and at the 10 MW prototype units at
Tennessee Valley Authority's Shawnee power plant near Paducah, Kentucky with
encouraging results.  The program at Southwest Unit 1 is the final step in
demonstrating adipic acid as an additive for commercial FGD systems.  At
the time of this writing, the demonstration program was in the second month
of a scheduled six-month program.

Test Program Objectives

     EPA objectives in this program are to confirm the results of their
previous testing and successfully transfer this technology from the pilot
and prototype stages to a full-scale limestone FGD system operating in both
a forced oxidation and natural oxidation mode.  City Utilities Southwest
Unit 1 represents a nearly ideal system for accomplishing these objectives
                                     339

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for the following reasons:

     the station fires high sulfur bituminous coal;

     the FGD system already includes a thickener, a  vacuum  filter,
     and a clay-lined landfill which are typical of  current dewatering
     and waste disposal techniques;

     the potential exists to increase S02 removal, improve  limestone
     utilization, and increase the efficiency of the dewatering  train;

     the unit is a commercial scale power plant that will require
     relatively minor modifications to perform the test program,
     thereby resulting in the most efficient use of  EPA funds.

     City Utilities expects to gain valuable information on the  operation
and performance of its scrubber.  Its objectives in  the program  are three
fold:

     aid in the successful completion of the demonstration
     program by providing the host site;

     evaluate the operating and cost advantages and
     disadvantages of adipic acid addition and forced
     oxidation at the SWPP scrubber;

     investigate the ability of adipic acid addition
     to keep the unit within compliance with the SO
     New Source Performance Standards.

     Anticipated advantages that City Utilities will see in their scrubbers
operation following adipic acid addition include:

     increased SO  removal, and

     improved limestone utilization.

Increased SO2 removal has several potential benefits with respect to operation
of the scrubbers.  First, the pH of the liquid in the outlet duct should
show a substantial rise above the normal range of 1.0 to 1.5.  In fact, a
sample of this liquid has been tested during the recent preliminary adipic
acid testing and its pH has been found to have increased to 3.7.  This is
due to the lower gas phase SO2 concentrations in the outlet duct.  Liner and
duct corrosion rates should therefore be decreased for this reason.  In
addition,  potential exists for removing some of the  ball charge  in each
scrubber and still having high enough removal to keep the unit in compliance.
Removing balls would have two positive affects.  First, the pressure drop
through the scrubbers would be decreased resulting in lower power costs for
the I.D. fans.  Secondly, a smaller ball charge would mean  less  chance for
pluggage due to ruptured or deformed balls; thereby  improving scrubber avail-
ability.
                                     340

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     The increased utilization of limestbne is also expected to result in
certain system operating improvements.  First, there should be less dissolution
of limestone on the TCA beds and demisters, therefore decreasing the potential
for scaling.  Also, fluctuations in SO  removal efficiency caused by varia-
tions in routine process conditions may be reduced due to the buffering
capacity of the adipic acid.  These advantages will be compared to the
additional operating cost incurred by adding the adipic acid.

Participants In Demonstration Program

     The Environmental Protection Agency has funded the development work
on adipic acid as an additive to limestone FGD systems.  This program
represents the agency's final step in upgrading the technology to commercial
status.  John Williams is acting as the project officer for the EPA Indus-
trial Environmental Research Laboratory (IERL) at Research Triangle Park  (RTF)
in this demonstration program.  The EPA contracted Radian Corporation to
conduct the test program and provide the necessary FGD expertise to evaluate
the program results.  Radian has subcontracted City Utilities of Springfield,
Missouri and UOP's Air Correction Division to provide the test site and
support for the necessary system modifications.

     As prime contractor, Radian's responsibilities in this demonstration
effort include overall project management and coordination, conceptual
design of the forced oxidation and adipic acid feed systems, development
and.implementation of the test program, evaluation of results, and reporting.

     Air Correction Division will prepare a detailed design and specifica-
tions for the forced oxidation and adipic acid feed systems; review quotes
and select vendors; and procure, install, and start-up the involved equip-
ment.

     The primary responsibilities of City Utilities in this demonstration
program include power plant and scrubber operation, review of proposed site
modifications, coordination of site modifications and interfacing with both
Radian and UOP during onsite testing.

Proposed Test Plan

     The adipic acid demonstration program will be divided into two test
phases.  The first phase will be a series of tests in the natural oxidation^
mode (present equipment configuration),.  Prior to the second test phase, V$\e
system will be modified so that air can be introduced into the reaction tank
for forced oxidation testing in Phase,II.

     Within each of these phases, a one-month duration test without adipic
acid (baseline test) will be conducted followed by two months of testing
with adipic acid.  Thus, the total program duration will be six months:
three months in the natural oxidation mode and three months in the forced
oxidation mode of operation.
                                     341

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      The  current plan  is to  conduct  this  baseline natural oxidation test
 during August,  1980.   This will document  the manner in which the system
 presently operates.  The scrubbing system will  follow boiler load during
 this  period and several fairly short-term tests will be conducted at various
 pH  levels.  However, most of this month will be used to monitor the system's
 operation as City Utilities  normally operates it.

      Following  this initial  baseline test,  adipic acid will be added to the
 system, and the effects on system performance will be monitored.  Two weeks
 of  adipic acid  testing are planned between  September 1st and 15th, when a
 one month scheduled outage will begin.  An  additional six-weeks of testing
 with  adipic acid in the natural oxidation mode  of operation will be conducted
 after the outage.  The forced oxidation baseline testing should be conducted
 in  December, 1980, with two  months of adipic acid-forced oxidation tests
 planned for January and February, 1981.

      The  adipic acid will be added to the limestone sump with the limestone
 from  the  ball mills as shown in Figure 4.   An on-off controller tied to the
 limestone feed  rate to the ball mills will  insure  that the  desired amount of
 adipic acid is  maintained in the reaction tank.   This desired adipic acid
 concentration can be altered by changing  the flow  rate from a weigh feeder.
 Adipic acid inventory  in the weigh feeder will  be  maintained from a system
 consisting of a vibratory hopper and screw  feeder.   The adipic acid concent-
 ration in the reaction tank  slurry will be  analyzed periodically to insure
 that  the  desired adipic acid concentration  is being maintained.

      The  oxidation air will  be introduced through  a sparger network consist-
 ing of PVC pipe in the reaction tank.  The  sparger pipe will be located fairly
 close to  the walls of  the rectangular reaction  vessel to minimize chances of
 damaging  the agitator  shaft.  The sparger ring  will be installed during the
 September outage to minimize downtime.  Four 1800  SCFM compressors will be
 utilized  to supply air to both reaction tanks.   An oxygen to SO  sorbed
 stoichiometry greater  than 2.5 can be maintained at full load with this air
 rate.

      Since this program is a demonstration  program rather than a research
 program,  only a minimum of parametric testing will be performed.   However,
 changes in scrubber feed pH, adipic  acid  concentration,  and air/SO2
 stoichiometry will be made to find the optimum  operating conditions within
 each  test phase.  Optimum performance will  be evaluated by  examining such
 parameters as SO2 removal efficiency, limestone utilization,  required adipic
 aicd  feed rate  (unaccounted  for losses of adipic acid),  and sludge dewatering
 properties.

 Preliminary Test Results

     The  initial results of  the adipic acid testing in early September
were very encouraging.   Prior to the  addition of adipic  acid to S-l module,
 its SO^ removal efficiency had averaged about 65 percent at the  normal
operating pH of 5.5.   After  addition  of adipic  acid to a liquid phase
concentration of between 800 and 1000 ppm,  the  removal efficiency of the
module increased to above 90 percent with a high of 95 percent at high
                                     342

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              FLUE GAS
            FROM BOILER
GO
£  COMPRESSORS
                 AIR FOR
            FORCED OXIDATION
                      TO
                  DEWATERING
                                        TO
                                      STACK
                                       i
                                   V
                                    HOLDTANK
       THICKENER
       OVERFLOW
                                                 RECYCLE
                                                  LIMESTONE
                                                     FEED
  AIR
SPARGER
                                                                  ADIPIC
                                                                   ACID
                                                                    r
                             BALLMILL
               LIMESTONE
              SLURRY SUMP
                                      LIMESTONE
                                        701913-1
                         Figure 4    Southwest Unit 1 Adipic Acid Test Program Flow Diagram.

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load conditions.  Improvements in limestone utilization were  also  noticed.
Results of a later test at an operating pH of 5.0 and an adipic  acid
concentration of 1500 ppm showed greater than 90 percent S02  removal
with limestone utilization of 99 percent.  Testing is scheduled  to begin
again after the maintenance outage.

CONCLUSIONS

     City Utilities is continuing its efforts to improve the  availability
and reliability of Southwest Unit 1 FGD Systems.  Corrosion and  absorber
area pluggage remain to be major problems to overcome.

     The use of adipic acid as a limestone additive appears to provide
an interesting alternative to be considered while evaluating  improvements
in system operation.  Improved limestone utilization and SO2  removal will
provide an economic basis for comparison with other potential alternatives.
                                     344

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ACKNOWLEDGMENTS

     The authors would like to acknowledge several individuals who
contributed their efforts in this endeavor.

     Bruce T.  Stone, P.E.
     Manager,  Power Production and Electric Distribution
     City Utilities; Springfield, Missouri
     R. Dean Delleney
     Program Manager
     Research and Engineering
     Radian Corporation; Austin, Texas
     John E. Williams
     Project Officer, Adipic Acid Test Program
     Industrial Environmental Research Laboratories
     U. S. Environmental Protection Agency
     RTP, North Carolina
     Walter C. Hauer, Operations Engineer
     Douglas M. Kinney, Maintenance Engineer
     0. C. Smith, Training Coordinator
     and other staff and clerical personnel at
     Southwest Power Station
     City Utilities; Springfield, Missouri
                                      345

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                RESULTS  OF THE CHIYODA THOROUGHBRED-121
                         PROTOTYPE EVALUATION
                           Thomas  M.  Morasky
                            Project Manager
                   Electric Power  Research Institute
                             Palo  Alto,  CA
                           David P.  Burford
                           Research  Engineer
                    Southern Company Services  Inc.
                            Birmingham,  AL
                            0.  W.  Hargrove
                            Senior Engineer
                          Radian Corporation
                             Austin,  Zexas
                               ABSTRACT

   A ten-month  evaluation of the Chiyoda Thoroughbred 121  Prototype ee
   Process  (CT-121)  was  conducted at the Sholz Electric Generating
   Station  of Gulf Power Company.  The 23-megawatt CT-121  prototype
   was  modified from existing CT-101 process  equipment at  Scholz  by
   Chiyoda  International  Corporation, a subsidiary of Chiyoda  Chemical
   Engineering  and Construction Company, Ltd.   Chiyoda operated  the
   prototype, and  the Electric Power Research  Institute and  Southern
   Company  sponsored technical  evaluations  of  the prototype  process
   performance.  This paper summarizes the  findings of these evaluations
   Detailed results  of the gypsum stacking  evaluation will be  presented
   with the Chiyoda  Thoroughbred 121 presentation.
Preceding page blank
                                   347

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                      RESULTS OF THE CHIYODA THOROUGHBRED-121
                                PROTOTYPE  EVALUATION
INTRODUCTION
The Flue Gas Desulfurization Program area of the Electric Power Research  Institute
(EPRI) is charged with responsibility of identifying,  evaluating,  and  advancing
FGD technology to help the electric utility industry meet current  sulfur  dioxide
emission standards in the most efficient, reliable, and economic manner.  The
Chiyoda Thoroughbred-121 (CT-121) system was reported  to offer technical  and eco-
nomical advantages over currently available flue gas  (FGD) desulfurization tech-
nology.  As a result, the EPRI and Southern Company Services sponsored  a  program
to have Radian Corporation of Austin, Texas evaluate the Chiyoda Thoroughbred-121
(CT-121) process.  (The Southern Company is an electric utility holding company
operating in the Southeast.  It includes Alabama Power Company, Georgia Power
Company, Gulf Power Company, Mississippi Power Company, and Southern Company
Services, Inc.)  As part of this program, Chiyoda  International Corporation, the
American subsidiary of Chiyoda Chemical  Engineering and Construction Company of
Japan, built and operated a prototype (23 MW) CT-121 process at Gulf Power
Company's Scholz Power Station near Sneads, Florida with the cooperation  of Gulf
Power Company.  To a large extent, this system was constructed by  modifying the
existing CT-101 demonstration equipment at Scholz.   The CT-121 process at Scholz
is designated as a prototype because it was the first  lar^e-scale  application of
the CT-121 process.

SYSTEM DESCRIPTION
Figure 1 shows a schematic of the Scholz prototype CT-121 plant.   This  system was
designed to treat 53,000 standard cubic feet per minute (85,000 normal  cubic
meters per hour) of flue gas (23 megawatts of electrical production at  Scholz).
However, during the test program, gas flows ranging from 25,000-55,000  scfm were
studied.

As shown in the figure, the inlet gas was cooled and saturated liquid  stream in a
venturi before entering the met bubbling reactor (JBR) where the bulk  of  the S02
removal  occurred.  Compressed air was injected into the JBR to completely oxidize
                                         348

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                                                                                      LIMESTONE
                                                        SCRUBBED Q AS
                                                       TO MIST ELIMINATOR
                                       Ftue a AS
V0
VENTURIPRESCRUBBER WITH
 KNOCK-OUT TANK (S3 ai>)
                                            OXIDATION AIR
                                    Figure 1.    Simplified process  flow diagram of Scholz prototype CT-121
                                                  flue gas  scrubbing  system.

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the sorbed S02 and to assist the agitator in maintaining  a good gypsum solids
suspension in the slurry.  From the JBR, the gas  passed through a mist eliminator
prior to exiting the system through a glass reinforced plastic  stack.   There was
no reheat provision in the prototype system.  Powdered limestone was slurried and
added to the JBR to control pH.  Limestone grinding  facilities  were not included
in the prototype.  The gypsum produced during the  evalutibn program was diposed of
in a gypsum stack, a disposal technique commonly  used in  the phosphate fertilizer
industry.  Basically, a gypsum stack is a free  standing body in which  solid-liquid
separation is achieved by solids settling in a  hollowed out section on top of the
stack.  The supernatant liquid flows through the  walls of the stack to form a
"moat" around the stack.  This disposal was evaluated independently by Ardaman &
Associates of Orlando, Florida under EPRI research project 536-3 during the CT-121
demonstration.  (A copy of the report was distributed at  the EPA symposium as an
unpresented paper.)

The unique and central feature of the CT-121 process  is the jet bubbling
reactor.  Figure 2 shows a schematic of the prototype JBR configuration.   SC^
removal, sulfite oxidation, limestone dissolution, and gypsum crystallization
reactions are all accomplished within this one  vessel.  This concept deviates from
the conventional limestone system which contains  large recycle  pumps,  separate
absorption vessels and reaction tanks.  Such a  scheme can affect the capital cost
of a FGD system.  In the JBR, the gas is dispersed several  inches beneath  the
slurry.  This minimizes the liquid phase mass transfer resistance which can limit
S02 removal in conventional spray tower systems.   The liquid pumping power
requirements are also low in the CT-121 system  because large slurry recirculation
pumps are not used, however, the power required to overcome the high gas side
pressure drop tends to offset this savings somewhat.  Figure 3  shows the physical
arrangement of the JBR, the inlet and outlet ducts and mist eliminator at  Scholz.

TEST PLAN AND OBJECTIVES
The objective of the program was to evaluate the  performance of the CT-121 system
under a wide range of operating conditions and  to  measure the reliability  of this
prototype.  By varying both site-specific and some non-site-specific parameters,
an "operating envelope" in which the CT-121 system can function successfully was
determined.  This performance evaluation therefore provides a basis for cost
evaluation activities as well as for some of the  design parameters required for
commercial  units.
                                          350

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c*>
                        FLUE GAS OUT TO
                        MIST ELIMINATOR
                 FLUE OAS IN FROM
                VENTURI SCRUBBER
                  (SaS5,OOOSCFM)
                    PRESCRUBBER
                     SLOWDOWN
                      (0-30 QPM)
                   POND RECYCLE 	£
                  WATER 15 20 QPM)
                                                                                              pH METER
                                                                                                                    	1
OVERFLOW TO
OYPSUM TANK
  (a 10 QPM)
* LIMESTONE
   TANK
                                                                                                                   LIMESTONE
                                                                                                                  SLURRY FEED
                                                                                                      BOTTOMS TO GYPSUM
                                                                                                        TANK (MO QPM)
                                    Figure  2.    Schematic  of  jet  bubbling reactor  (JBR).

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   JBR-i
Mist eliminator —i
Outlet duct.
   to stack
Figure 3.  Jet bubbling reactor, gas ducts, and mist eliminator.
                                352

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The testing of the prototype  CT-121  system was divided into four phases:
   Q    Phase 0   - Three-month duration startup, shakedown, and
                    initial  parametric tests conducted by Chiyoda.
   o    Phase I   - Two-month  duration baseline tests conducted at
                    Chiyoda  specified operating conditions to quantify
                    some  of  the control  variable fluctuations that
                    might be encountered during routine operation.
   o    Phase II  - Four-month duration test series conducted under a
                    variety  of operating conditions (forced variable
                    perturbations)  to evaluate system response under
                    operating  conditions that may be representative of
                    a  broad  scope of utility applications.
   o    Phase III - Three-week duration tests conducted by Chiyoda
                    following  modifications to the JBR internals to
                    simplify the JBR design and reduce capital cost.

 In all,  a  total  of ten  months of tests were conducted over an eleven-month period
 beginning  in  August  1978.   Throughout the program locally hired personnel, oper-
 ated  the system.  Chiyoda  provided supervision only during the day shift.  Chiyoda
 conducted  Phase  0 with  no  input from EPRI although operating data were transmitted
 to EPRI.  Phases I and  II  constituted the EPRI evaluation program.  During these
 phases,  the test conditions were proposed by Radian and approved by EPRI, SCS, and
 Chiyoda; an on-site  Radian test crew conducted the tests and reviewed operating
 conditions with  Chiyoda personnel.  During Phase III, Chiyoda performed the test-
 ing independently, but  Radian observed the testing as EPRI's and SCS's representa-
 tive.

 TEST  RESULTS
 Synopsis
 When  judged by five  critical  performance criteria:  S02 removal efficiency, solid
 waste'quality, limestone utilization, resistance to chemical scaling and reliabil-
 ity,  the performance of the CT-121 process throughout the EPRI evaluation program
 was quite  good.   S02 removal  efficiencies of 95 percent with an inlet flue gas
 concentration of 3500 ppm  S02 were achieved, and the gypsum produced throughout
 the program settled  rapidly and dewatered easily.  The operation of the prototype
 system was particularly outstanding  from the standpoint of limestone utilization
 and chemical  scale control.   Limestone utilization within the JBR averaged over
 98% for  the evaluation  program.  A detailed inspection at the conclusion of
 Phase  II revealed only  minimal  chemical scale deposition, none of which posed a
 significance  operating  problem.  This was after nine months of testing including
                                          353

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three months of Chiyoda shakedown operation and  six  months  of EPRI-sponsored
tests.  These performance results are excellent  in  view of  test conditions which
deviated significantly from Chiyoda's design  operating  set  points.   These results
thus  indicate that the system is flexible and can withstand significant process
upsets.  These results demonstrated that Chiyoda prototype  CT-121  is an FGD capa-
ble of continuous, reliable, and efficient operation.

SQo Removal.  The JBR overflow pH and JBR WP  influenced  the S02 removal  efficiency
to the greatest extent in the test program.   The S02 content of inlet flue gas
showed a marked effect on removal efficiency  only at concentrations  above
2200  ppm.  The oxidation air stoichiometry and flue  gas  flow rate  altered S02
removal characteristics of the JBR chloride levels up to 6000 mg/1 did not have a
measurable effect on S02 removal efficiency.

Three parameters, pH, WP, and inlet S02 concentration were  fit to  a  theoretically
derived expression for S02 removal efficiency.  The  basic form of  the mathematical
equation was initially derived by Chiyoda in  1978.   Tests varying  sulfur dioxide
(0/S02) stoichiometry and gas flow were fairly short term in nature  and were not
varied in conjunction with variations in other process conditions.   Because of
this  these were not included in the mathematical model for  predicting S02 removal.

The 229 data points used for this analysis were best fit by using  two equations,
the first for inlet gas S02 concentrations less than 2200 ppm and  the second for
higher S02 levels.  The primary reason for using two equations is  that nearly all
the testing was at an S02 concentration less than 2200 ppm  (200 data points).  A
single equation predicted accurate results for S02 levels less than  2200 ppm bu1:
did not adequately predict the removals observed at  higher  S02 concentrations.
Therefore, another set of equation coefficients were determined to better fit the
data at higher S02 concentrations.
                                          354

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e
Equation 1 predicts the  removal  for inlet S02 levels less than 2200 ppm whi
Equation 2 describes the results achieved at the higher concentrations for the
prototype CT-121 system.
                                              WP  l'Q7
                              1  - exp (-3.49]\hir70    I
    Fractional S02 removal  =  - ±2±2 - '  -  -          (1)
    (for inlet gas S02                 .,15.4, Min-pHmtr°2 „
    concentrations less      1  + 56'9 ^wF° N1°   ONTOOO°
    than 2200 ppm)
                              1  -  exp (-3.
     Fractional S02  removal  = - ±2i-i -      -      (2)
     (for  inlet gas  S02         ,                     S0
     concentrations  greater    1  +  .84 N^~~
     than  or  equal to  2200 ppm)          w

where WP is the JBR  pressure drop  expressed as inches of water, S02 is the inlet
flue gas sulfur dioxide  concentration in ppm and the pH is that measured at the
JBR overflow.  Both  of the equations are applicable only to the range of Phase II
test conditions at full  load gas flow and with 0/S02 stoichiometric ratios greater
than 8.  Figure 4 is a plot  comparing the measured removal with the values gener-
ated by these two equations.

The equations show the importance  of the pressure drop and S02 concentration pH,
on removal.   As the  pressure drop  increases, the exponential term decreases, thus
predicting a  higher  S02  removal.   Likewise, as the pH increases, increased S02
removal is predicted since both  equations'  denominators approach unity.  Increases
in either  pH  or WP were  expected to improve S02 removal  efficiency.  Since
increased  pH  results in  decreased  S02 back  pressure in the froth zone, and
increased  WP  reflects  longer gas-liquid contact time and/or more efficient flue
gas sparging.  Figure  5  shows the  effects of tradeoffs between WP and pH on S02
removal with  the prototype unit.   In most situations, it will  be more desirable to
obtain'the required  S02  removal  by using higher pH due to the relatively low cost
of limestone.  This  should be evaluated on  a case by case basis, and caution must
be used to ensure that increased limestone  concentrations do not cause scaling
problems.

Further examination  of Equations 1 and 2 show that S02 concentration had minimal
effect on  S02  removal  when the inlet S02 concentration remained below about
2200  ppm.  Above this  level, increases in S02 concentration caused a fairly rapid
decline in S02-term  exponent in  Equation 2  and is shown in Figure 6.  This

                                         555

-------
   100
  \  V
    90"

-------
   400
   350  —
03

1
£ 300
o

-------
   100
•=.- 95
 CO

 s

 0
DC
 CM
o
CO

E
o
s
o>
Q.
90
    85
    80
                       Predicted by Equations E-2, E-3


               SI^'z3 95% confidence limits of equation


                       95% confidence region of single observations
       0      400    800	1200	16QQ_   2000	2400

                          Inlet SO2 Concentration (ppm)
                                                        2800    3200
       Figure 6.  Fractional SOo removal versus input SO2 with fixed pressure drop

                (AP=11.5", pH = 3.5).
                                  358

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drop-off in S02 removal occurs  at an  S02  concentration higher than in many spray
tower designs mainly because of the increased liquid surface renewal  rate and
increased interfacial mass transfer area  created by the JBR design.

Even though the flue gas flow  rate and  the oxidation air rate were not included in
the predictive equations, these variables had a measurable impact on  the S02
removal rate.  The boiler variable load tests in Phase I indicated that flue gas
flows lower than 30,000 scfm resulted in  an average removal of 94% from a flue gas
containing 1000-1200 ppm S02 concentration.  Flows of above 45,000 scfrn during the
variable load test period resulted in an  average removal of 90 percent.
Unfortunately, there was not sufficient time to test the impact of low gas flows
at different pH's, WP's, and S02 concentrations.

The results of several short duration tests emphasized the importance of maintain-
ing rapid oxidation to achieve good S02 removal in the JBR.  These short-term
tests quantified the effect of air-rate (stoichiometry) on S02 removal as shown in
Figure 7.  While no difference between air rates of 1000 and 1300 scfm (1600 and
2090 Mm /hr) (0/S02 stoichiometric ratios ranging from 8 to 11) was seen in the
initial tests, Figure 7 shows  a reduction in S0? removal efficiency to about
                                             o *-
77 percent at an air rate of 480  scfm (770 Nm /hr)•(0/S02 stoichiometry of about
4).  With the air shut off, the S02 removal dropped to below 40 percent.  In addi-
tion to the 0/S02 stoichiometry,  distribution of air in the JBR (which is
influenced by such factors  as  air  sparger, agitator performance and specific craft
tube design) is also important in  maintaining good sulfite oxidation
efficiencies.  These design factors were  not examined in detail in this evaluation
program.

Changes in limestone sources and  increased chloride concentrations in the JBR
slurry had no measurable effect on S02 removal.  The main difference between tne
Southern Materials Company  (SMC)  limestone and the Georgia Marble limestone was
the particle size since both were  high calcium limestones.  The specified SMC
limestone grind was 90 percent through 200 mesh (74)m) and the specified Georgia
Marble grind was 90  percent through 325 mesh (44)rn). ' The driving force for disso-
lution was sufficiently high at the low operating pH's in the CT-121 prototype for
limestone size to have nd effect  on S02 removal.  Likewise, spiking the system
with 6000 ppm chloride (added  as  CaCl2) had no effect on S02 removal.
                                         359

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0)
cc
 
-------
Changes in the JBR configuration made  by  Chiyoda prior to Phase III  appeared to
have only minor effects on S02  removal  efficiency.   Removal  efficiencies of only
one to two percent lower than those  calculated  in Phase I and II  were calculated
even though flue gas velocities through the sparger openings had  increased
40 percent.

Limestone Utilization.  Throughout the program  the observed  limestone utilization
in the CT-121 system was quite  high.   For both  Phases I and  II, the  utilization
measured around the JBR remained above 98 percent.   Changing the  JBR overflow pH
from 2.5 to above 4.5, and the  limestone  grind  from 90 percent less  than 325 mesh
(44)m) to a grind of 90 percent less than 200 mesh (74)m) did not cause a
measurable change in utilization.

The utilization was also good even when one considers the limestone  added to the
gypsum tank for final  neutralization of the gypsum slurry to a pH of 6.  Optimiza-
tion of this  process step was not an objective  of the program.  The  limestone flow
to the gypsum tank was only  occasionally  adjusted because there were no on-line ph
monitors or controllers on the  gypsum  tank.  The samples taken during Phase II
indicated that the overall utilization including the neutralization  tank, was
somewhat lower in Phase II (f93 percent)  than in Phase I (f97 percent).  However,
it appeared that the multiple changes  in  process conditions  which occurred in
Phase  II may  have caused some pH upsets in the  gypsum tank.   This was probably the
primary cause of the lower utilizations.

During Phase  III, Chiyoda tested JBR overflow pH set points  approaching six.  At
these conditions, the  utilization in the  JBr dropped to about 87  percent.

Solids Characteristics/Gypsum Scaling  Tendency.  The solids  produced in the JBR
during the evaluation  were generally greater than 97% gypsum.  There were no sul-
fite solids measured since the  pH was  always low enough that calcium sulfite would
remain in solution until it  was oxidized.  Also, as discussed in the preceding
limestone utilization  section,  there were only  small amounts of calcium carbonate
remaining in  the JBR underflow  slurry.   The gypsum solids settled very rapidly
with no measurable differences  in the  free-fall characteristics between samples.

Figure 8 shows typical differences between solids formed when testing with lower
sulfur coal (nominal 1.8 percent sulfur)  and those formed with higher sulfur coal
(nominal 3.2  percent sulfur).   The crystals formed when cleaning  the flue gas from

                                         361

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               JBR underflow solids 11/29/78
                   1.8 percent sulfur coal
                JBR underflow solids 4/13/79
                   3.2 percent sulfur coal
Figure 8.  Comparison of solids produced with two SO2 loading.
                            362

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the lower sulfur coal were  long  rod-shaped crystals.  Many were over 400 microns
in length with length-to-diameter (L/D)  ratios of from 10 to 20.  The crystals
produced with higher sulfur loadings  were less than 100 microns with L/D ratios of
from 2 to 5.  This difference  is consistent with what would be expected from oper-
ation with higher sulfate liquor loadings caused by the higher sulfur coal.

Operation with higher sulfur coal  also increased the relative supersaturation of
gypsum in the JBR although  scaling conditions were not noted during the program.
The maximum  relative saturation  measured, even during S02 spiking experiments
(3000-3500 ppm S02 concentration), was only 1.23.  ;This is well beneath the crit-
ical level of 1.3 which  has been identified as the threshold for incipient
scaling.                                            '•',

Inspections  at the conclusion  of Phases I and II revealed little scale deposition
in the JBR.  There were  some random patches of gypsum scale on various surfaces,
but  none of  the depositions were threatening systemi performance and the scale
thickness was less than  1/16 inch (2  millimeters).  Since the scale buildup was
minimal, infrequent  routine cleaning  might be necessary since the scale deposition
will be a continuing phenomenon.  The duration between system cleanings was not
determined in the evaluation program, but it can be noted that nine months of
operation were logged and  no operating difficulties-were experienced.

Gypsum Disposal.  Throughout the program the gypsum was disposed of in a stack
which  is a disposal  technique  commonly used for gypsum produced in the phosphate
fertilizer industry.  Figures  9  and 10 show the stack during the initial fill
period and in the final  configuration.  Chiyoda also tested the product for use in
wallboard and Portland cement  production.  U.S. Gypsum and National Gypsum ooth
made successful production  runs  of over 100 tons each with gypsum produced by the
CT-121 prototype system.   Laboratory  tests also indicated that CT-121 gypsum could
be used successfully in  Portland cement.  Details of the gypsum disposal testing
will be the  subject  of a paper available with the handouts of this symposium.

.EPA Performance Parameters. The four performance parameters employed by EPA to
measure an FGD system's  dependability are presented in Table 1.  The overall
figures include both the Phase 0 shakedown and the Phase III test period.  Both of
these periods involved some planned outages which penalized both the operability
and utilization factors.  However, during the EPRI program, all four factors were
extremely good.  There were only 22 hours of forced outages during the EPRI evalu-
ation program.  Of this, 21 hours were due to limestone feeder problems.
                                         363

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Figure 9.  Stacking pond at start of Program 11/15/78.
                        364

-------
Figure 10.   Filled stack, end of Phase II 5/22/79.
                         365

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                                       Table 1

                             CT-121 VIABILITY PARAMETERS
Viability Parameters (percent)

Chiyoda Shakedown Phase
(Phase 0)
EPRI Evaluation Program
(Phases I and II)
Extended Chiyoda Testing
(Phase III)
Total Program Average
Availability3
99.2
99.3
99.5
99.3
Reliability5
99.1
99.3
99.1
99.2
0 per ability0
88.0
97.3
58.6
90.0
Utili:zationd
88.0
97.3
58.6
90. G

aAvailability - Hours the FGD system is available  for  operation (whether operated or
 not), divided by the hours in the perid.

Reliability - Hours the FGD system was operated divided  by  the hours  the FGD system
 was called upon to operate.

C0perability - Hours the FGD was operated divided  by the  boiler operating hours in
 the period.
 Total  Program = 6552/7276

"Utilization Factor - Hours that the FGD system operated  divided by total hours in
 the period.
 Total  Program = 6552/7276
                                       366

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When inspection time was added  to  the  total  downtime, the fraction of the periocj
in which the FGD system operated was 97.3 percent as reflected in the utilization
for Phases I and II.

These performance parameters  indicate  the CT-121 prototype performed with
exceptional reliability during  the evaluation program.  These figures cannot be
used to accurately predict  the  performance of a commercial system, but the evalu-
ation program indicates that  a  properly designed CT-121 system could be expected
to operate with a minimum  of  process or mechanical  problems.

Mist Eliminator Performance.  The  mist eliminator performance during the program
deserves special mention.   The  mist eliminator was composed of two banks vertical
Chevron blades mounted  in  a horizontal run of duct downstream of the JBR.  This
mist eliminator was washed  on an average of once a week for one minute with about
              o
300 gpm 0.072 m/s of pond  water.   No  signs of gypsum scaling or plugging were
noted during the program.

This excellent performance  is attributed to two major factors.  First, the super-
ficial gas  velocity leaving the froth  zone of the JBR was only about 2 ft/s
resulting  in most of the entrained slurry being separated from the flue gas in the
interior of the JBR or  in  the JBR  outlet gas chamber.  Secondly, the slurry con-
tained very little solid phase  alkalinity (CaCO, or CaSOo).  Therefore, the dis-
                                               0        O
solution of calcium solids  and  sorption of SC^ on the mist eliminator blades which
has caused  scaling problems in  many systems did not occur in the CT-121 prototype,

Overall System Controllability
The effective performance  of  the prototype system during the evaluation program
was .due to  (1) the flexibility  of  the  prototype to withstand process fluctuations,
and (2) the controllability of  the prototype system.  Two key process control
variables are monitored in  the  CT-121  system to ensure good performance:   (1) JBR
overflow pH and (2) JBR overflow solids concentration.  pH was used as the primary
control for S02 removal efficiency.

pH was continuously monitored with a dip-type sensor in the overflow weir, and
limestone  feed rate was manually adjusted based on this reading.  A neoprene wiper
was used, to keep a stagnant film from  building up around the probe.  This instru-
ment was checked daily and  calibrated  weekly.
                                         367

-------
pH fluctuations remained within ±0.2 units even after  flue  gas  flow rate
changes.  Operation in the 3.0 to 4.5 pH range resulted  in  rapid  limestone disso-
lution and good pH control.

The solids inventory in the JBR underflow was monitored  by  a  nuclear density
meter, and the gypsum discharge rate from the JBR was  adjusted  based on the solids
concentration.  Every four hours the operator checked  the instrument by taking a
slurry sample and measuring the volume of the'settled  solids.   Although the solids
content did vary somewhat from the set point, deviation  from  this  set  point did
not cause scaling during the program.  This was true even though  the solids con-
tent was reduced significantly for a period of several hours  during  two different
short-term tests.

It is also noteworthy to mention that locally hired operators were employed to
actually run the process (2 operators per shift) and Chiyoda  personnel were pres-
ent only during the day shift for most of the program.   The process  operated with
a minimum of problems or upsets using this approach to operator staffing.

SUMMARY
As a result of the independent evaluation program and  related engineering activ-
ities, several CT-121 process design and operating features have  been  identified
which may result in improved operability and reduced operating  costs  relative to
existing lime/limestone systems:
    o    no large slurry recirculation pumps,
    o    no nozzles or screens,
    o    high limestone utilization,
    o    less dependence on limestone source and size  on operation due
         to the low operating pH,
    o    low slurry entrainment in the gas enhancing mist eliminator
         performance,
    o    low scrubber profile which may lower capital  costs and,
    o    the ability to operate successfully over a wide range  of
         operating conditions with a minimum of scale deposition.
                                         363

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The concept of the JBR,  therefore,  represents a potentially attractive alternative.

to other currently available  FGD technologies.   The prototype at Scholz was suc-

cessfully tested  over a  ten month period and was shown to operate reliably and

efficiently under a  variety of test conditions  while treating flue gas from a
coal-fired utility boiler.


REFERENCES

1. Randall E. Rush  and  Reed  A.  Edwards.  Evaluation of Three 20 MW Prototype Fl ue
   Gas Desulfurization  Processes.   Final Report.  Birmingham, AL:  Southern
   Company Services, Inc.  March 1978.   EPRI No. FP-713-SY, EPRI Project No.
   RP536-1.

2. H.  Idemura,  T. Kanai,  and H. Yanagioka.  "Jet Bubbling Flue Gas
   Desulfurization." Chemical  Engineering Progress.  February 1978.  P. 46-5.0.

3. D.  M. Ottmers, Jr.,  et al.  A Theoretical and Experimental Study of the
   Lime/Limestone Wet Scrubbing Process.  Austin, TX:  Radian Corp.  1974.
   EPA 650/2-75-006, EPA  Contract No. 68-02-0023.
                                          36S

-------
                 Forced Oxidation of Limestone Scrubber Sludge
                   at TVA's Widows Creek Unit 8 Steam Plant
                                      by

                   C.  L.  Massey,  N.  D. Moore, G.  T.  Munson,
                        R.  A.  Runyan, and W.  L.  Wells

                          Tennessee  Valley Authority
                            Chattanooga, Tennessee
                                   ABSTRACT
     Tests on one module (140 MW) have been carried out to demonstrate the
feasibility of forced oxidation of limestone scrubber sludge to gypsum as a
viable technique for ultimate disposal of these waste materials.   Both one-
tank and two-tank oxidation experiments were studied with data indicating the
two-tank runs more closely met test objectives.  Equations to predict oxida-
tion were developed and expressed as a function of mass transfer and chemical
kinetics.  Air stoichiometries of between 1.75 and 2.0 Ib atoms 0/lb mole SC>2
absorbed will consistently produce oxidation of ~95%.

     As a result of the Forced Oxidation Test Program, this method is being
given consideration as one of the alternative methods of scrubber sludge dis-
posal for Widows Creek units 7 and 8.  Additionally, Paradise Steam Plant
units 1 and 2 scrubber trains are being designed with a forced oxidation
option to produce a sulfate waste product.
  Preceding page blank
                                      371

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                 FORCED OXIDATION OF LIMESTONE  SCRUBBER SLUDGE
                   AT TVA'S WIDOWS CREEK UNIT 8 STEAM PLANT
INTRODUCTION

     TVA uses, or plans to use, limestone wet  flue  gas  scrubbing as  the method
of reducing S02 emissions at two of  its  twelve coal-fired steam-electric gen*
erating plants—Widows Creek units 7 and 8  and Paradise units  1 and  2.  At the
remaining ten coal-fired plants, Widows  Creek  units 1-6,  and Paradise unit 3,
TVA burns either low- or medium-sulfur coal, or washed  coal to achieve the
required S02 emission limitations.

     Forced oxidation will be utilized in the  disposal  of the  sludge at the
Paradise plant.  The scrubbers are scheduled to become  operational by September
1982.  Forced oxidation is presently being  compared and evaluated with other
sludge disposal methods at Widows Creek.  The  total life-cycle costs of forced
oxidation sludge disposal will be compared  with total life-cycle costs of the
alternatives of raw ponding, mixing the  sludge with dry fly ash, and mixing
the sludge with dry fly ash plus additives.

     The future role of forced oxidation depends primarily on  the following:-

     1.   Technical feasibility of the process.

     2.   The total life-cycle costs of  forced oxidation  as compared with
          other disposal methods.

     3.   The final requirements of the  Resource Conservation  and Recovery Act
          (RCRA) on disposing of scrubber sludge.

BACKGROUND

     For the last several years, TVA has been  involved  in an intensive research
and development project which was initiated to make a thorough and complete
assessment of its first full-scale scrubber system  at Widows Creek unit 8,
located near Stevenson, Alabama.  The research and  development effort con-
sisted of six tasks which were designed  to  evaluate the scrubber system.  This
paper will report results of the forced  oxidation experiments  at Widows Creek
unit 8.

     The wet limestone scrubber system,  designed and constructed by  TVA, treats
flue gas from a 550-MW Combustion Engineering  (CE)  tangentially coal-fired
boiler.  The flue gas desulfurization (FGD) system  consists of four  parallel
scrubber trains, each capable of scrubbing  25  percent of  the flue gas.  Only
one of the four scrubber trains, train D, was  used  for  the forced oxidation
demonstration experiments.  Assistance in identifying the design criteria for
the test program of the forced oxidation demonstration  was obtained  from the
studies performed at the Shawnee Test Facility.

     TVA contracted with CE to install forced  oxidation equipment on the FGD
system at the Widows Creek Steam Plant to demonstrate that forced oxidation  of
FGD wastes is possible at this location  as  a processing scheme for waste
                                      372

-------
disposal.  The  forced oxidation demonstration program began on April  2,  1979,
and continued until November 15, 1979.   CE  had the responsibility for the  ini-
tial operational phase through June 30,  after which Radian Corporation assumed
the operatipnal responsibility through November 15, 1979.

     A flow schematic of Widows Creek Unit  8 Wet Limestone Scrubber System is
shown in Figure 1.   The pressurized scrubber system consists of four
                             STEAM
      TO ASH
      DISPOSAL PONO
      TO STACK PLENUM
                         2\
                                       AIR HEATER COILS
                                                                AIR FROM
                                        AIR HEATER FAN
                                                               POWER HOUSE
                                                                              -o
                                    -ENTRAPMENT
                                     SEPARATOR


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It
>>
*!
|.
, X
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                                                                       RIVER
                                                                    ^ WATER PUMPS


                                                                   FROM POND WATER
                                     RECYCLE PUMPS


                                          FROM
                                                                               O
    cc
      FROM ESP
     FROM B, CaD TRAIN

     'VENTURI CIRC TANKS

       TO SLUDGE
                    FAN
        POND
VENTURI CIRC   A0SORB£R CIRC
TANK 8 PUMPS   TANK & PUMPS
                 EFFLUENT SLURRY
                 SURGE TANK  & PUMPS
                                     LIMESTONE
                                      SLURRY
                          LS SLURRY  STORAGE TANK
                          FEED PUMPS
  SLUDGE POND
                      Figure  I.   Scrubber  System  Flow  Diagram
 identical trains located downstream of low efficiency  (approximately 50 per-
 cent)  electrostatic precipitators.   The principal components  in each train A,
 B,  C,  and D include a boiler I.D.  fan, venturi scrubber,  grid-type spray tower
 absorber, Chevron-type entrainment separator, indirect  steam  reheat system,
 venturi  slurry recirculation system,  and absorber slurry  recirculation system.
 Each module is capable of treating approximately 25 percent of the boiler flue
 gas at full load.

     The waste slurry produced by  the FGD system currently is stored in a 110-
 acre pond.   Disposal of this slurry represents a major  problem in continued,
 long-term operation of the scrubber unit.  It was decided to  evaluate and
 demonstrate the forced oxidation method for treating the  sludge to decrease
 the effective volume required for  disposal or to improve  the  stability of
 material in the disposal area.  During the demonstration  program, a forced
                                       373

-------
 oxidation system was installed on scrubber  train D.   Approximately 10 percent
 (4,370  Ib/hr of solids) of the oxidized  scrubber bleed stream was processed
 through a 2-stage dewatering system consisting of a  thickener and rotary drum
 vacuum  filter.   A flow schematic of the  demonstration unit is shown in
 Figure  2.  Initially, the filter cake from  the vacuum filter was reslurried
 COMPRESSED
            ABSORBER
            CIRCULATION
            TANK
                                                  THICKENER
                                                  UNDERFLOW
                                                  PUMP
                           RESLURRY TRANSFER
                                     TANK
                                                               EFFLUENT SLURRY
                                                               SURGE TANK
              Figure 2.  Forced  Oxidation  Dewatering  Equipment
and disposed of  in  the  pond.   After the test objectives  had  been achieved and
conditions determined for producing a cake of consistent quality,  arrangements
were made to initiate a landfill disposal project for  long-term monitoring of
the final product.  The gypsum produced at Widows Creek  is unusual in that 30
percent of the solids is fly  ash.   The presence of this  ash  may have as yet
undetermined effects on the long-term stability of the final disposal material

     Oxidizing air  was  introduced  to both the venturi  and absorber tanks by
means of a circular sparge ring, located just beneath  the agitator impellers
as shown in Figures 3 and 4.   Air  was discharged through thirty-six 1-1/4-inch
holes on the outside of the sparge ring (Figure 5).
                                      374

-------
on
Z <+
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I
                                                      33'-0"
                                               -BAFFLE
                                               16" O.D. PIPE
Figure  3.   Venturi Tank Agitator      Figure  A.   Absorber Tank Agitator
         and Sparge Ring                          and Sparge Ring
                                     (36VI 1/4" DIA. AIR DISCHARGE -
                                        HOLES ON OUTSIDE
                                          OFRINO
                    Figure  5.   Absorber Tank  Sparge Ring
                                      375

-------
Objectives and Goals

     The general objectives of the test program were  as  follows:

          Demonstration of forced oxidation as a viable  FGD  waste disposal
          option.

          Acquisition of data applicable to the design of  a  forced oxidation
          system for the Widows Creek units 7 and  8 FGD  systems.

     Three specifically quantitative goals of the  demonstration program were
as follows:

          Attainment of greater than 95 mole percent  conversion of calcium
          sulfite to sulfate.

          Production of a waste product capable of being dewatered to greater
          than 80 wt percent solids with a vacuum  filter.

          S(>2 removal efficiency of 88 percent or  greater.

     Originally, the test plan for the forced oxidation  experiments was divided
into three separate test blocks.  One test block (experiment B) was designed
to verify the hypothesis that the air stoichoimetry required for  oxidation in
the venturi effluent hold tank only would be significantly less than in the
absorber tank.  Results of this type have been observed  at the Shawnee test
facility.  However, such was not the case due presumably to  excessive carry-
over of venturi-loop liquors into the absorber loop.  This carryover appears
to be a function of boiler load (gas velocity) and results in either a leve-
lized pH in both tanks or inversions such that the absorber  tank  actually had
at times a lower pH than the venturi tank.  Oxygen stoichiometry  requirements
are closely related to pH.

     A second test block (experiment C) involved oxidation in both the venturi
and absorber hold tanks simultaneously to determine if such  dual  tank oxidation
could be accomplished at a lower oxygen stoichiometry than single tank oxida-
tion.  A third series of runs (experiment A) with  oxidation  in the absorber
tank only was cancelled because of the difficulties experienced with one tank
(venturi) oxidation as described in experiment B above.

Test Description and Results

     Operating conditions were varied to meet the  three  goals of  primary inter-
est.  Oxidation, dewatering, and SOg removal were  each studied with minimal
interference from the other parameters.  To determine the  minimum amount of
air necessary to achieve 95-percent oxidation, an  initial  air rate was chosen
which was known to give about 99-percent oxidation.   The air rate was then
reduced stepwise until oxidation was consistently  above  95 percent. After
tests at several air rates which gave between 91 and  99  percent oxidation, it
was possible graphically to determine the minimum  air stoichiometry.
                                      376

-------
     The air stoichiometry was then held constant at this value while the
dewatering train was tested.  This involved determination of the appropriate
combination of feed rate, filter area, drum speed, and filter pressure that
produced a product containing a minimum of 80 percent solids.

     Since the FGD unit is a commercial system, it was difficult to vary a
large number of operating variables to increase S02 removal.  In addition, TV*
was simultaneously involved in a comprehensive test program aimed at improving
the S02 removal of the "Widows Creek FGD system. " It was felt that the results
of this companion program could be applied to a forced oxidized system as well
as the existing system.  Consequently, only two variables were examined in
regard to S02 removal:  Ca/S ratio and the effect of additional packing in the
absorber.  Testing of these two parameters was sufficient to produce the
desired 88-percent S02 removal.  During the S02 removal tests, the forced oxi-
dation unit was operated to further refine the operating parameters.  The
equipment was operated in combination to demonstrate that the FGD unit and oxi-
dation unit could produce oxidized sludge of the desired quality while meeting
the S02 removal requirements.

     Operating parameters were set on the desired conditions and a period of 8
hours was used to allow steady state operation before sampling.  Usually only
one sample per sample point per day was drawn and analyzed.  An additional 12
to 14 hours of operation was required to verify steady state conditions and to
obtain a second set of chemical data.  A summary of sample data and analytical
determinations is given in Table 1.
                         Table 1.  Summary of Analyses
Saaple - Phase
Liquid




Solid




Slurry



Bleed Streaa
SO? Ca**
SO,
XCH
ci~
coT
soT
soC
COi
Mg
Anions Na+
K+
NHt
Anions Mg**



Cations


Cations

Acid Insoluble Quantity
Wt 2 Solids

PH
T«p
Settling Rate
Test






Thickener Underflow





so"
S0~

Acid





Ca++ )
( Cations
Anions Mg I

Insoluble Quantity
Particle Size Distribution
Wt Z
»H
Trap
Solids


Filter Uaf
Teat
Thickener
Overflow





X Solids




ull
Tenp


Vacuum
Filter Drum





Z Solids
Thickness on








l
i
Absorber bottoms
SOT Co"
SO^ Mg '
NOT Anions Na Cations
Cl Kf
COT Nut
soT j c*"
SOT Anlona MS" Citl°n6

Acid Insoluble Quantity
Wt 2 Solids

|)ll
Teap


     The following methods were employed to determine quantitatively cations
and anions of both solid and liquid samples.
                                      377

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Cation Analyses

     Analyses for calcium, magnesium, sodium, and potassium were done by atomic
absorption spectrophotometry.

Anion Analyses

     The analyses for the anions required a number of  different  analytical
methods.  These methods included:
          Ion chromatography for sulfate and chlorine  determinations.
          lodometric "back" titration with iodine for  sulfite  determinations.
        •  Nondispersive infrared (NDIR) analysis for C02  determinations.

     A representative set of operational and chemical  data  collected during
the demonstration is shown in Table 2.

               TABLE 2.  BLEED STREAM ANALYSIS AND TEST RESULTS
Liquid Phase
  Date
Time
  Test
Condition
Temp
 °C    pH   80s
                                                  Milligrams/liter
SC-4   Cl"  C03  Ca++ Mg++
12/20/79  0745
          C5
              41
       5.7   19   1278  1021  144  770  163
Solid Phase
                                              Milligrams/gram  solid
Test Venturi
Date Time Condition pH
12/20/79 0745 C5 5.7
Test Results

Ca++ S03 S04 C03 Mg
177 3 303 91 3

Relative Relative % Residual
saturation saturation electroneu-
CaS03'^H20 CaS04-2H20 trality

0.2 0.7 -3.6
CaC03 S02 Oxygen
added absorbed added
Ib-mol Ib-mol Ib-atoms
min min min
Comments

Steady state
0/S02
ratio Percent
Ib-atoms oxidation
Ib-mol
++ Acid
insoluble
279

Ca/SO
ratio
Ib-mol
Ib-mol
1.4
Vacuum
filter cake
% solids

 2.2
    1.3
          2.8
                                          2.3
                          99
                   86.8
                                      378

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CHEMISTRY OF FORCED OXIDATION

Proposed Reaction Mechanisms

     6xidation may best be explained in terms of mass transfer and chemical
kinetics.  The oxidation of sulfite to sulfate can be affected by several
chemical phenomena including gas absorption, reaction kinetics, dissolution
of solids and precipitation of solids.  The overall reaction,
       CaS03 + ^02 -»• CaS04                                         (1)

can be broken down into several steps, each a necessary link of the reaction
pathway and, as such, each a potential rate limiting step.  These are shown in
Table 3.
      TABLE 3.  REACTION STEPS AND PHENOMENA INVOLVED IN SULFITE OXIDATION


           Reaction Step                   Phenomena Involved


     Dissolution of reactants      Gas absorption, solids dissolution

     Reaction                      Kinetics

     Precipitation of products     Solids precipitation
     First, it is necessary for the reactants to be in the liquid phase.  This
 involves absorption of 02 by the scrubbing liquor and either dissolution of
 solid calcium sulfite or absorption of S02 as indicated by reactions (2)
 through (5).

          02(g) -»• 02 (aq)                                              (2)

          S02(g) + H20 •* HSOs(aq) + H+(aq)                             (3)

          CaS03 • &i20(s) -» Ca++ + 80s + %H20                          (4)

          80s + H20 •» HSOa + OH*                                       (5)
     The oxidation reaction then takes place between the dissolved reactants
according to reaction (6).

          HSOs(aq) + V>2(aq) -> SO^Caq) + H+(aq)                        (6)
     Finally, the reaction product, gypsum, is removed  from the  liquid phase
by precipitation.

          SO^aq) + Ca*+(aq) + 2H20 •* CaS04-2H20(s)                    (7)

     The entire sequence is illustrated schematically in Figure  6 and each  of
these steps is discussed in detail in the following paragraphs .


                                     379

-------
                S02(g)
 GAS               \

   	V           ,	    -
 LIQUID               HS03  (aq)  + &)2(aq)	» S04~(aq) + H
   	/                 	V
 SOLID             /                                      \
              CaS03^H20(s)                              CaS04-2H20(S)

                Figure 6.  Mass Transfer  and Reaction Sequence


 Dissolution  of  Reactants
     Bisulfite, HSOg,  appears  to  be  the  reactive form of the dissolved
 hence  subsequent  discussion  will  refer to  bisulfite rather than sulfite which
 is  also  a  dissolved  species.

     Bisulfite can be  dissolved in the liquid phase by two mechanisms, absorp-
 tion of  SOg  from  the flue  gas  and dissolution of solid calcium sulfite.

     In  forced oxidation processes where oxidation takes place outside the
 scrubber circulation loop, dissolution of  calcium sulfite solids is clearly
 the predominant form of bisulfite generation.   Since the bisulfite is  being
 removed  by oxidation,  the  sulfite relative saturation is expected to be low
 (<1) and calcium  sulfite dissolves.

     The Widows Creek  demonstration  involved  oxidation within the scrubber
 loop.  In  this case, bisulfite ions  will be supplied by the absorber,  and dis-
 solution of  solid sulfite  will not be  of any  importance unless sulfite solids
 are precipitating in some  part of the  system.   During C-series testing,  air was
 sparged  into both hold tanks.  Figure  7  is a  plot of the relative saturation
 of calcium sulfite versus  percent oxidation in the solid-phase for the B and C
 series tests.
          RS               a
          K&CaS03-%H20 = - £

where
     a   = activity of subscripted component

     Ksp = s°lubility product of the precipitation  reaction (temperature
           dependent)

Note that for C-series tests (two tank oxidation) the  relative  saturation was
substantially greater than 1 at most oxidation  levels,  indicating that bisul-
fite ions absorbed in the scrubber were oxidized without  first  precipitating as
CaSOs'i^HgO-  This means that at intermediate oxidation levels,  oxidation com*
petes with precipitation for HSOs ions, and dissolution of  solid  sulfite is iiot
part of the reaction mechanism.  The low relative saturations seen at extremely
high oxidation levels are most likely due to sulfite ion  depletion,  caused by
sulfate precipitation and not any dissolution mechanism.

                                     380

-------
 12
    B SERIES TESTS - 0
        ONE-TANK SPARGING

 10 h c SERIES TESTS - A
        TWO-TANK SPARGING
O
in
o
O

&
 ' 6
Ifl

>4
s
           /
                                                                             I
                                                                         A ~ -
                                                                             A
                                                                        A
                           0  0                                       *    *   *
                                                                          \A^
                                                               o   °   o
                                                                          A
                                                                            *
0          A
                 J	I	I	1	1	1	1	1	$t
          10      20      30      40      50      60      70      80      90      100

               Mole % Oxidation = SO^/CSOa + 804)  in  solid phase
          Figure 7-  Relative Saturation of CaS03-%H20 vs  Oxidation in
               Venturi Hold Tank - One- and Two-Tank Air Sparging


      Relative saturation data for B-series tests  (one tank oxidation) indicate
 that dissolution may have been a more important factor in these tests.   With
 air introduced only into the venturi circulation  tank, CaS03*%H20 precipitat:.or
 would have been expected in the absorber  circulation tank, necessitating disso-
 lution in the venturi tank.  Also,  since  significant backmixing occurred
 between the two tanks, the dissolution step  has been made more pronounced as a
 source of calcium bisulfite than for a true  two-stage system with single-tank
 oxidation.

      In summary, this analysis indicates  if  the absorber  tank is  sparged, then
 the source of bisulfite is S02 absorption and  solids dissolution  is not neces-
 sary.  Therefore, solids dissolution can  be  eliminated as a potential rate lim-
 iting step in the C-series testing  described in this report.  However, this is
 not true for the B-series testing performed  earlier.  When just  the venturx
 tank is sparged, solids dissolution is a  necessary link  in the reaction pathway
 since the source of bisulfite resulting from S02  absorption is insignificant.

      Another step of the reaction pathway involving reactant dissolution is
 oxygen absorption.  This is primarily a mass-transfer process, affected by both
 chemical and mechanical factors.  The system chemistry affects two parameters

                                       381

-------
that are important to mass transfer:  oxygen  solubility  and the diffusivity of
dissolved oxygen.  Oxygen solubility decreases with  increases  in both tempera-?
ture and ionic strength.  The diffusivity of  dissolved oxygen  will  increase
with increasing temperature and decrease with increasing ionic strength.
Neither temperature nor ionic strength varied substantially during
demonstration testing.

     pH also has an important effect on the oxidation reaction in that oxi-
dation of sulfite causes the pH to rise when  in the  presence of excess limer
stone.  This increase in.pH will rapidly quench the  reaction unless  some
method of replenishing H  ions is available.  At Widows  Creek,  the pH level
for oxidation purposes was maintained by 862  absorption.

     Under normal operating conditions at Widows Creek,  with the pH  at 5 to 6,
the sulfite species are 40 to 70 percent in the bisulfite form.   This is suf-
ficient for forced oxidation.  The pH's of the two hold  tanks  rarely differed
by more than 0.5, but if the backmixing problem were eliminated,  the pH in the
absorber would be higher.  Since bisulfite availability  is  not rate-limiting,
the effect this would have on a force-oxidized system may be small unless the
pH was over 6.5.

     The data indicate that during the tests, pH values  were in the  proper
range to provide high concentrations of the bisulfite ion.   Therefore, bisul-
fite ion availibility can be eliminated as a  limiting step  in  the overall
reaction sequence.  The potential rate-limiting steps are thus  reduced to
reaction kinetics, product removal, or 02 transfer.

Reaction Kinetics

     Thermodynamics indicate that the oxidation (equation 5) reaction is essen-
tially irreversible, with an equilibrium constant (25°C)  on the  order of 1040.1
Therefore, we need only consider the kinetics of the forward reaction.

     Most forced-oxidation research has indicated that the  reaction  is rela-
tively fast.  If this is true, then the site  of the  reaction is  limited to the
gas/liquid interface.  This indicates that mass transfer to the film between
the gas and the bulk liquid will be the limiting factor,  and not reaction
kinetics.

     Using film theory terminology, the phase interface  and reaction zone of
the oxidation reaction can be shown by two models in Figure 8.   Model I illus-
trates a fast second order rate reaction where the diffusion rate of 02 and
HS03 in the liquid film are not limiting the  overall reaction  and the reaction
is fast enough so that the reaction zone remains totally within the  liquid
film.

     Model II shows an instantaneous reaction first  order rate expression where
the concentration of HS03 is relatively high  and the reaction  plane  is moved
to the gas-liquid interface.  The overall rate will  be limited by the diffusion
of 02 through the gas film.  The film models  shown in the figure result in
mathematical models for the reaction rate that are essentially the  same as
those for mass transfer without reaction, except for an  "enhancement" term.
Reaction in the film tends to thin the film,  and the enhancement term accouaU
for the corresponding increase in mass transfer.

                                     382

-------
        MOON. I:
SULK
QAS
           PO,
QAS
FILM
LIQUID
 RIM
BULK
LIQUID
Reaction only in film,  general fast-irreversible  reaction.
     R
                • reaction rate • K eaPOj
                - Gas- and liquid-side oxygen  mass-transfer coefficients

                • Henry's Law constant for  oxygen

                • Complex ^function of C...-.-, C..
                                       cloU 3   ^2
     a          • Interfacial area per unit  volume
     POa        • Gas-side partial pressure  0:

For an infinitely fast reaction,  the expressions become:
     R          • Kga E P02
                  \   I   ^ S(
               i -i
                   K       K •  v,
                  L o2g     Oti J
                -  1 + (constant)  <
                                     POi
.. ... 8ULX
ELII: GAS



PO,




GAS
flLM


.
\
\
\
>
LIQUID 1 8ULX
FILM | LIQUID
1
1
1
^- flEACTION ATINTEBFACE
.^ \
** \
\
\
I
                                                           CM483.(MiQW
Reaction only in film, high HSOj concentration,  general  fast-irreversible
reaction.
     R  - Kga ?02
     K  .1" _ 1_ + constant]
      5  LK02g   V^HSOj  J
For an infinitely fast reaction,  Che  expressions  become:

     R  - K    a ?02
       Figure  8.   Models for  Film Reactions2
                             383

-------
     The film reaction models  suggest  that mass transfer of 02 is the limiting
step rather than kinetic limitations .   This is  evidenced by the presence  of
the oxygen mass transfer coefficient in the expressions for reaction rate conr
stant.  Therefore, in terms of the  overall reaction rate, both sulfite and
reaction kinetics are not rate-limiting steps.   Sulfate precipitation rate does
not affect the kinetics and, as will be shown in subsequent discussion, will
be a function of the reaction  rate.  The most probable rate-limiting step "in
the overall reaction sequence  is then  oxygen transfer.  However,  data are
needed to confirm this and to  validate one. of the models shown in Figure. 11.

Removal of Products

     An important aspect of forced  oxidation is its effect on the relative
saturation of CaS04.  The relative  saturation for sulfate (RS) is defined
similarly to that for sulfite.


          RS             3Ca++ '
          KbCaS04-2H20 = -
                             SpCaS04-2H20

where

     a   = activity of subscripted component

     K   = solubility product of the precipitation  reaction (temperature
           dependent)

     RS of calcium sulfate is important because  it  can affect  scaling  of the
scrubber.  Generally, for 1 < RS < 1.3, crystal  growth will occur  on existing
gypsum crystals.  At RS > 1.3 gypsum nucleation  can occur  which can result in
crystal growth or scaling on the scrubber  internals.   This can eventually
require a shutdown to remove the scale.

     While forced oxidation increases the  total  amount of  S04  or CaS04-2H20
present, the RS., 0/.  01I _ at Widows Creek  was not increased and may have been
               LabU4 •
decreased.  This is attributed to the higher  sulfate  concentrations  resulting
in an increase in gypsum solids surface area  which will  enhance the  gypsum
precipitation rate.

     After the bisulfite is oxidized, it  is necessary to remove the  sulfate
product from solution.  This is accomplished  via precipitation of the sulfate
as solid gypsum, CaS04'2H20.  Gypsum precipitation has been studied  extensive 0
with respect to flue gas desulfurization  systems.  The driving force for preci-
pitation is relative saturation, and three regimes can be considered as shown
in Table 4.
                                     384

-------
   TABLE 4.   GENERAL EFFECT OF RELATIVE STATURATION OF GYPSUM PRECIPITATION

   Relative Saturation                           Effect


           <^                       Dissolution of gypsum solids
       !-° ~ I-3                    Precipitation on existing solids
          >l-3                      Solids riucleation
     A simple rate expression for gypsum precipitation can be written as

          r = KafC (RS-1)                                             (10)
where

     r  = precipitation rate (gram/liter-sec)

     K  = temperature dependent constant (gram/cm2-sec-unit driving force)

     a  = crystal interfacial area per gram of precipitation solid
          (cm2/gram)

     f  = weight fraction of the precipitation species in the solid phase

     C  = total solids concentration in the slurry (grams/liter)

     RS = relative saturation of calcium sulfate in the liquid phase

     The precipitation rate of CaS04 is a function of both total crystal sur-
face area and relative saturation.  At steady state the precipitation rate must
equal the oxidation rate.  From an operating standpoint, it is desirable for
the relative saturation to be kept below 1.3 to avoid scaling of the scrubber
internals.  In a design situation, the maximum relative saturation can be
limited by designing an appropriately sized reaction vessel.  A large tank
volume will give an equivalent precipitation rate at a lower relative satura-
tion.  However, in a retrofit situation, as exists at Widows Creek, the tar.k
volume is fixed, and either crystal surface area or relative saturation will
vary in order to provide the necessary precipitation rate.

     The relative saturation of gypsum in the venturi hold tank was approxi-
mately 1 during most of the forced-oxidation testing at Widows Creek.  This
indicates that a relatively small driving force (RS-1) was sufficient to keep
the crystallization rate equal to the oxidation rate.  This result might have
been anticipated because the available gypsum crystal surface area (afC) is
high.  The system may have benefited from the significant increase iu agita-
tion over nonforce-oxidized systems.  The increased agitation may increase
available crystal surface area by shearing existing crystals into smaller
ones.  Since a relatively small driving force Was sufficient to keep the
precipitation rate to equal the oxidation rate, this indicates that
precipitation was not a rate-limiting step.
                                     385

-------
Oxygen Transfer

     In a process consisting of  several  steps,  the rate of the limiting step
is essentially.equal to that of  the  overall  process.   In this case, if the
oxygen transfer rate is assumed  limiting and can be modeled, then the rate of

the overall process will be known.   Furthermore,  this analysis can determine
which are the significant variables  affecting this critical path.  This infor-
mation will allow accurate decisions to  be made with respect to improving the
sulfite oxidation step and perhaps yield data useful in applying forced oxida-
tion to limestone scrubbers of different configurations.   The analysis approach
and results are presented in the following section.

Data Analysis

     The preceding discussion of chemistry and  mass-transfer theories suggests
several variables that may have  an effect on oxidation rates, since the reaction
is apparently mass-transfer limited,  and the variables that most directly affect
mass-transfer should be of primary importance.   These would include the partial
pressure of oxygen, the concentration of HSOs,  and mass-transfer coefficients.
Also, pH, temperature, and ionic strength could be expected to affect the oxi-
dation rate because of effects on oxygen.solubility and sulfite concentration.

     Table 5 presents some of the variables  calculated in order to model the
forced oxidation process.  The oxidation rate (R)  calculation and the net air
stoichiometry (AS) calculation account for a 32 percent "baseline" or "natural"
oxidation that is not due to air sparging.   The gross air stoichiometry (FAS)
calculation implicitly assumes 100 percent forced oxidation and no baseline
oxidation.  Consequently, AS will be a somewhat higher number than FAS.  FAS
is the air stoichiometry usually presented in the literature when forced
oxidation is discussed.

     Two general types of models were examined,  mass  transfer and overall
oxidation rate.  The first type  involved correlating measured and calculated
variables with the corresponding calculated  mass  transfer coefficient (K a).
                                                                         O \
The second type involved correlating measured and calculated variables with
the calculated oxidation rate (R).

     Several data fits were made based on these models, in order to determine
the most accurate representation of  the  Widows  Creek data.   The results of the
correlations of the data obtained during the demonstration are inadequate to
model the rate of the oxidation  process.  This  is not surprising when the
nature of the data is considered.

     Attempts to model the forced-oxidation  system at Widows Creek were compli-
cated by several problems.  Modeling the reaction was not a program objective.
and, therefore, no attempt was made  during demonstration testing to vary impor-
tant parameters systematically over  a broad  range.   Also, there was no reliable
means of monitoring continuously the flue gas flow rate due to high grain load-
ings which plugged probes.  Rather this  was  estimated by correlating fan amps
                                      386

-------
               Table 5.   Variables  and Units  -.Oxidation Modeling


R
Variable
Oxidation Rate
("Forced")
Units
Ib-mole S
min
Source


Ox     Net Solid-Phase


K a    Mass-transfer
 6     Coefficient

AS     Net Air Stoichiometry


FAS    Gross Air Stoichiometry


COi    Partial Pressure 02
      (log man)


POj In  Partial Pressure Oi
      (bottom of lank)

POi out  Partial Pressure Oj
      (top of tank)
                          mole Z
                   Uol
                                                  moles S0t
	  Ib-roole 0;	 F	
•in-f>-(psi driving force) I (tank.
   es, SO3 + moles SO.,

     Air x (0.791)(scfm)
                                    x 100"j ln 3Olid-phase analysis
    Ib-atoa 0 in
Ib-mole S force-oxidized

  Ib-atom O in
Ib-mole S removed

psi



psl


psi
     volume f3) x Avg Pressure (psi)

[[Air x 0.209) scfa x 2 atom/mole Oa "1
 379 f'/lb-mole x R Ib-mole S/min  J

[(Air x 0.209) scfm x 2 atom/mole Os"|
Fliie Gas (scfm) x AS022 removal  rate
calculations, oxidation rate calculations, and. air Stoichiometry calculations
and, as a  result, errors or inaccuracies in the flow rate measurement impact
these other variables as well.   Therefore, accurate flue gas flow rate  measure-
ments are  critical if an accurate model of oxidation rate is desired.

     Oxygen partial pressure was not measured directly,  and oxidation rate
could not  be measured directly.   Because of this, oxygen partial pressure,  oxi-
dation rate, air Stoichiometry,  and mass-transfer coefficients were calculated
from a mass balance involving  flue gas flow rate, oxidizing air flow rate,  SOa
removal, and oxidation.  Because all these factors could only be calculated
from the same base data, it was  not possible  meaningfully to correlate  them
against each other.

     Figure 9 is a plot of solid phase oxidation versus  air Stoichiometry.
While the  rate does not appear to vary with Stoichiometry in any consistent
manner, it is possible to draw some conclusions concerning net oxidation.  It
shows when gross air  Stoichiometry was 2.0 or greater, net oxidation was con-
sistently  95 percent  or greater.  Thus, an air Stoichiometry of 2.0 to  2.1
could be considered a conservative guideline  for this agitator/sparge  ring
configuration.
                                        387

-------
   z
   o
   X
   o

   UJ
   I
   a.
   o
   CO
cr-

UJ
o
2
      100.0
       97.5
       95.0
       92.5
       90.0
       87.5
       85.0
       82.5
                           AAAAA  A   A     A  A

                              A   A A       A
                        A     A
                             A   A   A     A
                                 A  A
                                  A   A

                                     A   A
                  I
                     I
                                      I
I
           1.0    1.2     1.4     1.6 •   1.8    2.0    2.2    2.4    2.6    2.8

               GROSS  STOICHIOMETRY (FAS).  Ib-atom O/Ib-mole S removed


            Figure 9.  Solid Phase Oxidation vs  Air  Stoichiometry
     The analysis in the preceding section  suggests  that the oxidation reac-
tion is 02 mass-transfer limited.  Although the  data set was not suited to  for-
mulating a generalized model, mass-transfer principles  identify several factors
that will affect the process.  Air sparging rate and agitation are both very
important mass-transfer parameters, but  increases in either parameter will
result in increased capital and operating costs.
                                      388

-------
RESULTS AND CONCLUSIONS

     The following results and conclusions were reached at the conclusion of
this demonstration program.  The process areas covered include system chemis-
try, the oxidation reaction, and oxidation and dewatering equipment.   Most of
these conclusions are specific to dual-tank air sparging at Widows Creek.


          The reaction appears to be limited by the rate of oxygen mass trans-
          fer.   Neither bisulfite dissolution, reaction kinetics, nor gypsum
          precipitation is the rate-limiting step.

       •  During testing with air sparged in both hold tanks (C series),  S02
          pickup in the scrubber was the primary source of bisulfite  ions for
          the oxidation reaction.  When only the venturi tank is sparged,
          solids dissolution is a necessary link in the reaction pathway,
          though not necessarily a rate limitation.

       •  During dual-tank oxidation tests, bisulfite ion availability was not
          a rate-limiting factor, and the reaction was relatively insensitive
          to pH.  The pH should be maintained below 6.5 to keep sufficient
          bisulfite available for the reaction,

          S02 absorption in the scrubber is sufficient to maintain the pH in
          the proper range when oxidation, is performed within the scrubber
          loop.

       •  Forced oxidation did not cause gypsum scaling.  Gypsum relative satu-
          ration was only slightly greater than one during these tests, due to
          high availability crystal surface area.  Gypsum crystals existing on
          packing will tend to grow in both oxidized and unoxidized systems,
          resulting in scaling of the packing.  Forced oxidation will not
          eliminate maintenance or cleaning requirements for scrubber
          internals.

       •  Forced oxidation nearly eliminated solid calcium sulfite in the FGB
          waste at Widows Creek.  For solids samples that met the 95  percent
          oxidation criterion, mean calcium sulfite was less than I percent by
          weight.

       •  The gypsum particles fell primarily in the 20 to 100 pm size range.

       •  The results of testing could not be modeled accurately, largely
          because of inaccurate estimates of the flue gas flow rate.

       •  An air stoichiometry of 2.0 Ib-atoms 0/mole S02 absorbed provided
          consistent sulfite oxidation of >95 percent.

          Calculated thickener unit-area requirements for oxidized sludge are
          1.7 square feet per ton per day of solids or less.  A more conserva-
          tive figure should be used in design.  Settling-test results showed
          the compression point was 40 percent solids or greater.
                                     389

-------
       •  The small-scale thickener at Widows  Creek was underloaded,  and had
          an unreliable rake mechanism.   Its operation does not necessarily
          predict the operation of a full-scale  unit.

       •  The filter-sizing criterion for Widows Creek oxidized sludge is
          approximately 200 pounds of solids per hour  per square foot of clott
          based on industry experience.

       •  The small-scale filter at Widows  Creek was underloaded and  its opera
          tion does not necessarily predict the  operation of a full-scale unit

       •  Filter cake product of 75 to 85 percent solids was attained with
          forced oxidation.

       •  Forced oxidation did not significantly affect 863 removal.

          pH is too insensitive to dissolved limestone concentrations to be an
          effective control point for limestone  feed rate.

       •  Forced oxidation can result in  increased total dissolved  solids (IDS)
          in the scrubbing liquor as a result  of water reuse.

       •  The effects of increased TDS on the  Widows Creek system are not pres-
          ently known and should be studied prior to applying  forced  oxidation
          to these units.

REFERENCES

1.   Dean, John A., Editor.  Lange's Handbook  of Chemistry,  Eleventh  Edition.
     McGraw-Hill.

2.   Levenspiel, Octave.  Chemical Reaction Engineering,  2nd Ed., New York.
     John Wiley and Sons.  1972.

ACKNOWLEDGEMENTS

     The oxidation work was funded in part  by  the Environmental Protection
Agency, Industrial Environmental Research Laboratory,  Research Triangle Park,
North Carolina.

     Portions of this paper are taken from  the Combustion Engineering Environ-
mental Systems Division's Final Report, "Demonstration of Forced Oxidation at
TVA's Widows Creek 8 FGD System," dated December 7,  1979,  and  Radian  Corpora-
tion's Final Report, "Forced Oxidation Demonstration and Testing at Widows
Creek Steam Plant," dated July 18, 1980.  Both corporations were under contract
for various phases of involvement pertaining to  this TVA R&D project.

     The contents of this paper do not necessarily reflect the view and poli-
cies of the Tennessee Valley Authority, nor does mention of any trade names or
commercial products constitute endorsement  or  recommendation for use.

     The authors wish to express their appreciation to the following  persons
without whom this report would not be possible:   Jose  DeGuzman,  Jim M.
Cummings, and the Widows Creek Steam Plant  Management  and Staff.

                                  390

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                  LA CYGNE STATION UNIT NO. 1

              WET SCRUBBER OPERATING EXPERIENCE
                               by
                       Richard A.  Spring

             Superintendnent of Air Quality Control

                        La Cygne Station

                 Kansas City Power & Light Co.
In the  late  1960's,  Kansas City Power & Light Company and Kansas
Gas & Electric  Company entered into a joint venture to construct
an 800  MW coal  fired generating unit.  An east central Kansas
location  was selected for its ample coal reserves and adequate
water supply capabilities.

The coal  reserves  proved to be a low grade with an average of
5k percent sulfur  and 24 percent ash.  To make this coal an
acceptable boiler  fuel a large scale air quality control sys-
tem was required.  After considerable pilot testing on a
smaller generating unit burning similar coal, a venturi -
absorber  scrubber  using limestone as the scrubbing agent was
selected.  Construction of the La Cygne Station Unit #1 started
in April  1969 and  began commercial operation in June 1973.

This paper presents  a review of the operating experiences,
0 & M cost trends, availabilities, modifications, manpower
and other supportive data relating to this limestone scrubber
system.
                                391

-------
STATION DESCRIPTION
The 820-megawatt La Cygne No. 1 Unit began  commercial  opera-
tion on June 1, 1973, as a joint project of Kansas  Gas and
Electric Company and Kansas City Power and  Light  Company.
The companies share equally in ownership and output, and
the unit is operated by KCP&L.  The 630-megawatt  No. 2 Unit,
in service since being declared commercial  May  15,  1977,
operates under an identical arrangement.

The plant site is located about 55 miles south  of downtown
Kansas City, one-half mile west of the Missouri State  line,
and was selected based on locally available coal, water,
and limestone.  Construction of No. 1 Unit  began  in 1969
and erection of the Air Quality Control System  was  initiated
in mid 1971.

Water for cooling purposes is furnished from a  2,600 acre
reservoir constructed adjacent to the plant site.   Fly ash
and spent slurry from the AQC system is piped to  a  300 acre
settling pond located east of the reservoir.

Coal is delivered to the plant in off-the-road  120  ton
trucks from surface mines operated by the Pittsburg &  Midway
Coal Mining Co.  The nearby coal deposits are estimated
to contain 70 million tons.  The fuel is low grade,
sub-bituminous with an as-fired heating value of  9,000 to
9,700 Btu/lb. and an ash content of 25 per  cent and sulfur
content of 5 to 6 per cent (Table 1).

Limestone is obtained from nearby quarries  and  delivered
to the plant in off-the-road 50 ton trucks.

The boiler for No. 1 Unit is a cyclone-fired, supercritical,
once-through, balanced-draft Babcock & Wilcox unit, with
a rating of 6,200,000 pounds of steam per hour, 1,010
degrees F, 3,825 psig at the superheat outlet.  The turbine-
generator was supplied by Westinghouse and  is rated at 874
MW gross output with five per cent overpressure and 3,500
psi throttle pressure.  Three auxiliary, oil-fired  boilers
are used for plant start-up or for powering  a 20 megawatt
house turbine-generator.   The net plant output is  820 mega-
watts,  adjusted to include 24 megawatts used by the FGD
system and 30 megawatts by plant auxiliaries.

FGD SYSTEM DESCRIPTION

The La Cygne wet limestone FDG system (AQC)   consists of
eight venturi-absorber modules,  connected together  by  a
common inlet and outlet plenum,  capable of  treating
2,760,000 ACFM of boiler flue gas at 285°F.   The ductwork
design is such that flue gas  cannot bypass  the  system, but
                              392

-------
                       Table 1

                 LA G.YGNE STATION

               COAL AND ASH ANALYSIS
                       COAL
Proximate

Volatile
Fixed Carbon
Ash
Moisture
BTU/lb.
28.63
37.94
24.36
 9.07
                100.00
9421
Ultimate

Moisture
Carbon
Hydrogen
Nigrogen
Chlorine
Sulfur
Ash
Oxygen
  3.60
 51.93
  3.43
  0.94
  0.027
  5.39
 24.36
  5.33

100.007
Grindability
59.59
Analysis

Phosphorous Pentoxide
Silica
Ferric Oxide
Alumina
Lime
Magnesia
Sulfur Trioxide
Potassium Oxide
Sodium Oxide
Titania
Other
                        ASH
        0.15
       46.05
       19.23
       14.07
        6.86
        1.02
        7.85
        2.48
        0.60
        1.02
        0.67

      100.00
Fusion Temperature

Reducing I.D.   1957
   Soft (H=W)   2045
   Soft (H=W/2) 2169
   Fluid        2321
Oxidizing I.D.  2156
   Soft (H=W)   2338
   Soft (H=W/2) 2415
   Fluid
   2520
                          393

-------
each individual module can be  isolated  from the system
for maintenance.

The on-site limestone processing  facility  is composed of
two 110 ton/hr. wet  ball mills and  two 260,000 gal.  storage
tanks, capable of supplying up to 1,000 tons of slurry
per hour from 3/4 in. x 0 in.  limestdne.   This  slurry
is processed to consist of 20  per cent  solids by weight.

The unit is a balanced draft system  with three  7000  hp
forced draft fans and six induced draft fans located
between the AQC and the 700 foot  stack.

The spent slurry and fly ash is removed from the module
recirculation tanks thru rubber lined pipe to a 300  acre
settling pond at a rate of 3000 to 3500 tons per day.
Clear make-up water is pumped  from this pond for slurry
make up, sump pump operation,  and wash  water thus allowing
a closed loop operation.  (Figure  1)

The hot boiler flue gas first  enters the venturi section
(Figure 2) of the module and is sprayed with limestone
slurry in a concurrent manner  from 48 spray  and 32 wall
wash nozzles.  This results in agglomeration of up to  99
per cent of fly ash particles  which  is  collected in  the sump
below.  The flue gas then makes a 180 degree turn up
through two layers of stainless steel sieve  trays upon
which slurry is sprayed from 24 spinner vane nozzles.
At this point the SC>2 in the flue gas and  the calcium
carbonate in the slurry react  to  form two  relatively
insoluable salts, calcium sulfite and calcium sulfate,
which also fall to the sump.   The scrubbed flue gas  then
passes thru a series of demisters and is then reheated
before entering the induced draft fans.

OPERATING EXPERIENCE

As a result of the continuing  modifications  and improved
operating procedures, the module  availabilities have
steadily improved.  The annual averages  (Table  2) have been
31% for 1973, 76.3% for 1974,  84.3%  for 1975, 92% for  1976,
92.5% for 1977,  93.5% for 1978, and  95.1%  for 1979.  With
the addition of the eighth module in April 1977,  continuous
daytime load capability has exceeded 800 megawatts without
appreciably affecting average  module capability.

The results of a full load and stack emissions  test on
August 26, 1977, (Table 3) indicated module  gas flow was
still below crusing capability, the  induced  and forced
draft fans were loaded well beloW rating and most systems
were in good balance.  Sulfur  dioxide removal efficiency
                              394

-------
«D
                                            .* C^y^its  [-• r-'•*""

-------
                                      LACYGNE FGD  MODULE
   4500
   PPM
   REHEAT
    STEAM
     550

1000 PPM '
x-*- S02
' ' 190° f
REHEAT COILS 1

(0 0 Q O Q O

J*
X
^
s
s
~\
-43"
H20

                                         TO
                                                                       FAN
 HOT AIR
~ FROM
 BOILER
INTERMITTENT
OVERSPRAY
  2150 GPM

 CONTINUOUS
 UNDER SPRAY
   140 GPM
         VENTURI SPRAY
           WALL
           WASH
           SPRAY
                  /\ /\  /\
                                      V  V   V  V  V  V   V
     VENTURI
     THROAT
     FLUSH
            PREDEMISTER
                               ABSORBER
                                SPRAY
                                           1_JL i_l  __-_
                                           ABSORBER
                                           200-600 GPM
RECIRCULATION  TANK
                                          70 C/L
                                  CASO3  35 C/L
                                  CASO4 " 25 C/L
                                  FLYASH 40 C/L
                                  PH = 5 5- 6.0
                                  8- 10% SOLIDS
  SPENT SLURRY
   TO  POND
     700 GPM

 *3500 TONS/DAY
693000 TONS/ "EAR
453 ACRE FEET'YEAR
               VENTURI
            ^ECIRC.  PUMP
              5000 GPM
                                  ABSORBER
                                RECIRC. POMP
                                 9000  GPM
           FOR  ALL  MODULES
     Figure 2
        396

-------
                                            Table 2


                                MODULE AVAILABILITY SUMMARY  - 1973
MONTH
JANUARY
FEBRUARY
MARCH
APRIL
MAY
JUNE
JULY
AUGUST
SEPTEMBER
OCTOBER
NOVEMBER
DECEMBER
A





20
7
79
13
28
48
42
B





21
24
64
0
41
1
20
C





40
25
65
13
34
38
5
D





21
41
74
13
54
4
31
E





27
27
47
13
33
63
26
F





30
25
48
0
3
59
11
G





23
31
70
0
46
49
32

AVERAGE %
AVAILABILITY*





26
26
64
7
34
37
24
31%
NET MWH





87,529
90,669
250,319
20,073
117,106
104,255
61,013
BOILER
HOURS





294
303
699
95
452
463
339

GENERATION
LOAD FACTOR





15.2
15.2
42.1
3.5
19.7
18.1
10.3
17.7%
co
UD
   *MODULE HOURS

    HOURS IN MONTH

-------
                                         Table 2  (Cont'd)

                                 MODULE AVAILABILITY SUMMARY -  1974
MONTH
JANUARY
FEBRUARY
MARCH
APRIL
MAY
JUNE
JULY
AUGUST
SEPTEMBER
OCTOBER
NOVEMBER
DECEMBER
A
49
66

67
69
92
75
90
69
71
90

B
32
68

70
83
84
80
90
88
61
71

C
44
59

75
78
83
80
73
73
59
60

D
87
76

88
85
90
81
81
76
81
61

E
23
52

74
78
82
85
81
83
79
84

F
37
100

100
84
83
79
78
89
93
85

G
81
65

88
80
87
77
99
86
89
84


AVERAGE %
AVAILABILITY*
50
69

80
80
86
80
85
81
76
76

76.3%
NET MWH
35,862
85,256

83,880
157,949
185,473
110,122
231,382
209,127
230,302
130,128

BOILER
HOURS
364
364

332
500
480
313
571
606
662
386


GENERATION
LOAD FACTOR
6
16

15
27
32
19
39
36
39
23

25%
CO
l£>
00
   *MODULE HOURS

    BOILER HOURS

-------
                                         Table 2 (Cont'd)

                                 MODULE AVAILABILITY  SUMMARY - 1975
YIONTH
JANUARY
A

FEBRUARY
S1ARCH
kPRIL
YlAY
JUNE-
JULY
AUGUST
SEPTEMBER
OCTOBER
SIOVEMBER
DECEMBER
82.4

94.6
87.8
7 8 . 4
74.5
78.4
66.2
92.9
90.7
B
Turbii
Turbii
96.0
Generc
85.1
85.4
89.7
88.1
83.6
77.3
Gener<
90.8
Generc
87.4
C
le Gene
le Gene
89.5
itor Re
94.2
83.9
89.6
87.3
.84.4
46.3
ator Re
80.2
ator Re
80.9
D
:rator
>rator
76.6
E
Repair
Repair
93.0
:pair 25 Days
89.5
84.9
83.7
78.0
84.7
73.6
?pair '.
93.2
jpair !
85.2
89.8
84.1
85.4
92.4
78.8
71.9
.5 Days
96.1
L7 Days
86.9
F


91.5

89.3
86.1
87.4
85.0
77.8
73.1
89.4
88.6
G


96.0

83.4
88.6
85.2
83.1
74.2
64.7
93.9
83.7

AVERAGE
AVAILABILITY*


89.33

89.4
85.8
85.6
84.07
80.25
67.57
90.83
86.19
84.3
NET MWH

7,886
244,873
23,014
332,526
324,952
297,870
294,402
239,954
74,660
165,058
278,597
BOILER
HOURS


694

683
667
590
630
610
231
346
597

GENERATION
LOAD FACTOR


41.1
3.4
55.9
56.4
50.0
49.5
41.7
12.5
28.7
46.8
38.6
ID
   *WORK-ING HOURS  + RESERVE
      HOURS IN MONTH

-------
                                         Table 2  (Cont'd)

                                 MODULE AVAILABILITY SUMMARY  -  1976
MONTH
JANUARY
FEBRUARY
MARCH
APRIL

MAY

JUNE
JULY
AUGUST

SEPTEMBER
OCTOBER

NOVEMBER
DECEMBER
A
85.8
93.9
92.3
92.3

96.5

93.3
95.6
94.1


97.4

94.7
86.8
B
84.6
90.3
89.7
90.5
Schedi
92.1
C
90.7
85.8
88.4
88.7
D
71.8
91.2
93.0
97.1
E
83.9
91.7
94.2
95.8
F
82.3
93.1
91.3
98.0
aled Outage 24 Days
93.5
95.7
89.4
Scheduled Outage 9 Days
94.1
95.0
93.1
94.0
91.9
91.8
95.0
92.9
93.4
92.3
93.0
91.8
95.3

93.5
93.7
90.4
Turbine Repair, Stack Relininc
Turbine Repa
96.7
97.5
iir, St
89.0
:ack Re
96.1
Turbine Repair, Stack Re
93.3
88.5
93.7
81.0
95.3
93.5
94.2
93.6
ilininc
"
96.1
:lininc
91.3
94.7
G
84.3
94.6
91.4
94.8

96.2

90.6
94.0
87.6
AVERAGE
AVAILABILITY*
83.3
91.5
91.5
93.9

94.1

93.3
93.7
91.7
8 Days
30 Days
96.1
18 E
93.6
91.4

95.6
ays
94.0
89.9
92.0
NET MWH
301,641
308,361
337,468
76,810

223,048

320,701
359,028
275,014


88,925

342,236
358,338
BOILER
HOURS
620.5
594.5
643.0
143.0

436.3

656.0
688.3
521.0


255.8

626.8
706.3

GENERATION
LOAD FACTOR
50.6
55.4
56.7
13.3

37.5

55.7
60.3
46.2


14.9

59.4
60.2
46.4
O
O
   ^WORKING  HOURS -I- RESERVE
       HOURS IN MOiri'H

-------
                                      Table 2  (Cont'd)
                              MODULE AVAILABILITY SUMMARY - 1977
MONTH
JANUARY
FEBRUARY
MARCH
APRIL
MAY
JUNE
JULY
AUGUST
SEPTEMBER
OCTOBER
NOVEMBER
DECEMBER

A
94.2
93.4
94.0
96.1


95.0
88.9
93.2
90.7
93.1

B
90.0
93.0
92.2
93.7
C
95.0
92.6
85.9
97.0
D
95.1
93.8
94.3
94.2
E
94.5
93.3
91.4
95.2
Generator Repair And
Stack Relining - 63 Days
92.8
55.2
93.7
95.6
96.3
Turbii

94.4
93.2
89.1
89.3
93.4
ie Rep a

94.8 J94.6
93.1 J89.7
90.0
94.2
94.2
ir Nov

92.8
93.4
92.2
. 15 -

F
91.6
93.9
94.0
96.1


94.9
92.8
95.0
93.5
92.5
Dec.

G
89.8
88.0
90.1
94.5


95.4
92.9
91.7
88.5
95.5
25

H
	
	
	
	


95.4
93.3
93.0
93.0
95.1


AVAILABILITY*
92.9
92.5
91.7
95.2


94.6
87.4
92.3
92.3
94.0

92.5%
NET MWH
255,822
310,748
295,420
178,226


213,334
253,605
287,701
173,979
118,439

BOILER
HOURS
539
590
558
384


485
501
524
457
234


LOAD FACTO]
43.0
57.8
49.6
30.9


35.8
42.6
49.9
29.2
20.6

39.9
*WORKING HOURS  &  RESERVE HOURS
       HOURS  IN MONTH

-------
                                      Table 2 (Cont'd)
                              MODULE AVAILABILITY SUMMARY  -  1978
MONTH
JANUARY
FEBRUARY
MARCH
APRIL
MAY
JUNE
JULY
AUGUST
SEPTEMBER
OCTOBER
NOVEMBER
DECEMBER
A
90.2
92.4
95.3
91.4
88.9

87.9
92.1
96.1
95.9
91.7
93.9
B
94.8
93.4
95.2
92.1
91.5
OUTAG
97.2
92.5
96.0
95.5
94.9
92.9
C
94.6
95.1
90.4
92.8
91.6
D
95.1
94.3
95.4
90.8
93.1
E
93.4
90.6
94.4
90.2
91.5
F
93.5
96.9
94.7
91.8
90.6
E 6-8-78 thru 7-17-78
91.9
95.0
96.3
98.3
94.3
94.0
93.9
95.7
95.8
97.0
93.3
95.0
88.4
92.7
95.9
97.0
93.6
94.7
92.8
94.3
95.7
97.6
93.0
90.5
G
94.4
95.5
88.6
90.6
93.1

93.1
94.7
95.3
96.7
94.3
94.4
H
94.0
93.4
93.3
90.5
85.6

95.3
95.3
96.6
96.3
96.1
94.7

AVAILABILITY*
93.8
94.0
93.4
91.3
90.7

92.6
94.0
96.0
96.8
93.9
93.8
93.5
NET MWH
332,033
334,897
264,961
330,571
291,651

160,847
307,378
390,826
138,126
386,402
91,744
BOILER
HOURS
582
594
593
620
582
14
340
579
720
255
720
239

GENERATION
LOAD FACTOR
54.2
60.5
43.2
55.7
47.6
0
26.2
50.1
65.9
22.5
65.1
15
42.2
*WORKING HOURS  & RESERVE HOURS
     HOURS IN MONTH

-------
                                           Tabi-e 2 (Cont'd.)

                                  MODULE AVAILABILITY SUMMARY - 1979
MONTH
JANUARY
FEBRUARY
MARCH
APRIL
MAY
JUNE
JULY
AUGUST
SEPTEMBER
OCTOBER
NOVEMBER
DECEMBER
A
95.6
95
96.1
95.5
96.5

86.8
96
95.3

B
96.5
94.6
96.0
95.7
96.3
Outag
95.9
96.1
95.8
C
97.2
92.6
93.2
94.4
96.7
e May
96.3
95.6
94.7
Outage Oct<
I
D
96.3
93.5
95.6
91.4
95.3
26 - A
96.3
94.3
92.7
3ber 19
E
90.7
95.1
96.5
95.5
95.4
ugust
95.9
96.7
94.4
- Dec
F
97.2
94.3
94.8
96.2
95.7
16
96.2
96.1
94.9
. 31
G
97.2
94.1
95.7
95.9
96.3

88.5
96.0
94.7

H
95.4
93.8
93.4
95.7
95.5

96.9
96.9
94.5


SYSTEM
AVAILABILITY*
95.8
94.1
95.2
95.0
96.0

94.1
96
94.6

95.1
NET MWH
46,538
141,322
147,645
342,240
222,924

83,169
321,108
207,639

BOILER
HOURS
205
342
314
638
452

230
618
455


GENERATION
LOAD FACTO
7.82
26.29
24.81
59.43
37.45

13.97
55.75
34.89

32.55
o
CO
   *WORKING   HOURS & RESERVE HOURS

           PERIOD HOURS

-------
                                      Table 2 (Cont'd)
                              MODULE AVAILABILITY SUMMARY  -  1980
MONTH
B
D
   SYSTEM                  BOILER GENERATION
H  AVAILABILITY*  NET  MWH HOURS  LOAD FACTOR
JANUARY Outage January 1 - February 20
FEBRUARY 98.2 98.2 97.4 99.1 98.2 99.1 99.1 99.6 98.6
MARCH 94.6 96.2 96.1 96.1 95.8 94.7 93.3 95.7 95.3
APRIL 96.3 95.1 95 96.7 95.3 92.5 97.0 97.0 95.6
MAY 96.4 94.6 95.7 95.9 96.1 96.5 96.1 96.8 96.0
JUNE 98.2 98.0 97.4 98.1 98.1 98.3 98.7 99.3 98.3
JULY
AUGUST
SEPTEMBER
OCTOBER
NOVEMBER
DECEMBER

52,768 157 9.48
1,187 32 2.00
206,936 472 35.93
324,478 689 55.19
195,974 370 34.02






*WORKING HOURS & RESERVE HOURS
       PERIOD HOURS

-------
o
01
                                                Table 3

                                      LA CYGNE STATION  UNIT NO.  1


                              FOUR HOUR FULL LOAD & STACK EMISSION TEST
DATE: August 26, 1977
TIME: 11:00 A.M. - 12:00
LOAD RANGE: 800 + MW
AMBIENT TEMP: 94° F
MODULES A B
GAS FLOW INDICATED
THROAT POSITION
REHEAT TEMPERATURE
VENTURI P
REHEATER P
ABSORBER DEM. P
REHEAT OUTLET
DAMPER POS.
ID FAN AMPS
ID FAN INLET
DAMPER POS.
FD FAN AMPS
LAB pH
SULFITE g/1
CARBONATE g/1
S02 EFFICIENCY %
INLET (PPM)
OUTLET (PPM)
400
OPEN
170
5
2.5
6.5

50
380

42
490
5.45
60.4
50.3
80.0
4600
920
350
OPEN
190
5.5
5.5
5.5

100
420

42
470
5.7
72.4
75.6
82.1
4600
825
NOX EMISSION: 0.81 # mm BTU
Midnight AVERAGE SO2 REMOVAL: 77%
PARTICULATE EMISSION: .213 # mm BTU
C D E F G H
380
OPEN
150
5
4.5
10

96
380

32
430
5.55
101.0
53.1
74.9
4600
1150
400
OPEN
190
5
4-5
7.5

38
400

36

5.7
74.1
54.4
64.3
4600
2285
352
OPEN
185
5
5
7.0

100
470

36

5.58
70.0
59.4
76.4
4600
1085
380
OPEN
180
5
2.55
6.5

52
470

40

5.77
43.9
83.8
72.1
4600
1285
370
OPEN
160
5
4.5
8.0

100
(540

366
OPEN
170
5
5.5
7.0

100
MAX)

( % OPEN)
(540
5.72
43.9
68.1
73.1
4600
1235
MAX)
5.29
63.6
42.5
74.8
4600
1160

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                                       Table  3  (Cont'd)
        CONDENSER VAC  (IN. HG)                    2.5
        WINDBOX FURNACE DIFF. PRESS  (IN.H20)   	32_
        SCRUBBER OUTLET PRESS  (IN.H20)           -39"
        FURNACE PRESS  (IN.H20)                     -2
        F.D.  FAN DISCHARGE  (IN.H2O)                41
        PEND.  REHEAT GAS PRESSURE  (IN.H2O)         -5
        AIR FLOW (%)                               85
        BOILER EXCESS O2 (%)                      2.2
        BAROMETRIC PRESSURE  (IN.Hg)             29.01
        STACK GAS TEMP  (°F)                       209
        FLUE  GAS MOISTURE  (%)                   13.66
        STACK GAS VELOCITY Ft/Sec              103.15
PRIMARY SUPER GAS PRESS.  (IN.H2O)    -8
HORZ REHEAT GAS PRESS.  (IN.H2O)    -9.5
ECON OUTLET GAS PRESS.  (IN.H2O)    -11.5
FEEDWATER PRESSURE  (PSI)           4200
THROTTLE PRESSURE  (PSI)            3400
THROTTLE TEMP.  (°F)                1000°
HOT REHEAT TEMP.  (°F)              1300
FUEL FLOW %                          68
FUEL HEATING VALUE  (MTB)           9800
FLUE GAS VOLUME  (MCFM)             2998
STACK CO2 %                        13.4
STACK O2 %                          5.4
O
en

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averaged 77% with individual modules averaging from 65 to
80%.  Although particulate emissions from the plant have
met EPA and Kansas State requirements, research and
development work continues in an endeavor to reduce further
the particulate emissions from Unit #1.

Limestone utilization has greatly improved with improved
pH control.  In the past, it has been almost insurmountable:
to maintain inline glass cells without caking the limestone
during shutdown or abrading the cells during operation
with the high concentration of fly ash.  By centralizing
the pH monitoring equipment and backflushing the pH cells
with water for 5 minutes every eight hours "straight
line" pH is resulting in approximately 30% less limestone,
better control of scaling and has eliminated one more
variable which hinders analysis in other areas.

Demister pluggage or scaling is no longer a problem at
La Cygne.  By eliminating the intermittent wash and moving
the continous wash  (140 GPM) from below to above the first
demister with increased number of nozzles  (230 GPM),
the chevrons operate "squeaking clean".  Further experi-
mentation may allow a reduction in these nozzles and per-
haps sequential washing to reduce excess water.

Hard scale on the reheater tubes has been eliminated by
the addition of a second layer of demisters in each of the
modules.  Scaling of the reheaters continues to be a pro-
blem, however, it is soft and can be removed using fire
hoses.  The previous hard scale required high pressure
water to remove the deposits.

MAINTENANCE

Cleaning schedules continue to call for taking one module
out of service each night on a rotational schedule and
keeping all modules available for the daytime peak loads.
This allows a complete checkout of module internals to
clean steam reheater pluggage, check nozzles for debris
or  loose rubber pluggage, to clean sump accumulation and
to  inspect for any other maintenace that could reduce
reliability during the week.  Module inspection and
cleaning is now reduced to six hours or less with re-
heater pluggage the greatest problem.  Scaling is not one
of our chief problems and we ordinarily ignore soft scale
that forms on walls, on beams, or on the outside of
nozzles.

Carryover to the induced draft fan blades continues to
require regular washings.  Each fan now requires cleaning
once very four to seven days.  A "spinning" process
                               407

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with low pressure hoses has been very effective for cleaning
the spare fan while out of service.  The washings are
usually done on a preventative basis, but must be taken
out of service if bearing vibrations exceed 12 mils.

Rubber pipe linings and rubber-lined pumps have been an
increasing maintenance problem.  After several years
operation, some materials that haven't been modified are
wearing out.  Rubber linings that tear out cause damage
in other piping or pumps, plug nozzles and allow the steel
pipes to wear through.  This problem would not have been
classified as serious, but this very abrasive slurry in
practically continuous operation can be detrimental in
trying to attain higher module availability, so a preventa-
tive maintenance program to change the piping in critical
areas has been initiated.

Corrosion of carbon steel in the ductwork, dampers, in-
duced draft fan rotors and housings, breeching and stack
liner is and will continue to be our greatest concern.
A replacement program has been underway since the fall of
1979.  This program began at the outlet of the demister
section where the walls from this point to the reheater
section were replaced with 1/4" 316L  stainless steel.
In the reheater section replacement continued with the
duct from the reheat bundles to the module outlet dampers
being replaced with a coated carbon steel.  New module
outlet dampers have also been installed.  Future plans
include replacement of all the ducting from the module
outlet dampers to the induced draft fans, the induced
draft fans inlet and outlet dampers, induced draft fan
housings, and the ductwork from the induced draft fans
to the stack.

MANPOWER REQUIREMENTS

The scrubber operating and maintenance force has been
increased to 54 people by adding one electrician for a
total of two and a maintenance foreman to supervise both
electricians and technicians.  The remaining personnel
will remain the same (Table 4).

Also worth noting are the increased demands on present
maintenance personnel to accumulate, record and evaluate
operating data on water saturation trends,limestone
utilization, draft fan wear rates, reheater bundle failures,
lined pump failures, rubber lined pipe replacements,
nozzle replacements, spare parts, etc. for preventative
maintenance programs.   The operators are also busy up-
dating and extending operating instructions, special
instructions and reviewing safety and training procedures.
                               408

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                 Table 4
       LA CYGNE AIR QUALITY CONTROL
          MANPOWER REQUIREMENTS

           OPERATORS PER SHIFT
3 Attendants                    13
3 Clean-up                      14
1 Shift Foreman                  5
1 Process Attendant  (Chemist)    1
                                33
               MAINTENANCE
Mechanics                        8
Apprentice Mechanics             2
Welder                           1
Electrician                      2
Technician                       2
Plant Helpers                    2
Foreman                          2
                                19
              ADMINISTRATIVE
Superintendent                   1
Engineer                         1
                  TOTAL          54
                     409

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COSTS

The total cost of the FGD system to date has increased to
$55.1 million or 25% of the $216.3 million total Unit #1
cost.

The production costs for the La Cygne FGD system  (Table 5)
in 1977 was 1.7 mills/KWH and for 1979 it was 4.9 mills/
KWH.  This drastic rise is due to the increase in main-
tenance materials to repair the "cold end" corrosion
mentioned earlier.  Discounting escalation, future
production costs associated with the operating labor,
operating materials, and maintenance labor should re-
main the same or trend downward while the maintenance
materials will increase slightly.

CURRENT PROGRAMS AND PROJECTS

The major project concerning the FGD system, at present,
is the systematic replacement of the cold end duct
work mentioned previously.  To help combat this corrosion
problem, studies are continuing for increasing the reheat
steam supply.

Analytical programs to investigate the mechanics involved
with the scale formation at the various levels of the
scrubber modules and collection of sub-micron flyash
have been implemented.  Results of these programs are
currently under scrutinization.

Other areas of hopeful improvement are in the demister
section with the addition of a third layer, and on line
incline reheat tube cleaning.
                               410

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                                   Table 5 - LA CYGNE UNIT #1
                                  FGD  SYSTEM  OPERATING EXPENSE
OPERATING
LABOR

OPERATING
MATERIALS

MAINTENANCE
LABOR

MAINTENANCE
MATERIALS

LIMESTONE
      1973
DOLLARS-MILLS/KWH

$ 162,934 - 0.223


    3,480 - 0.005


  189,400 - 0.259


  441,737 - 0.604

  264,514 - 0.362
                                          1974
                                   DOLLARS-MILLS/KWH
                            1975
                      DOLLARS-MILLS/KWH
                          1976
                    DOLLARS-MILLS/KWH
$ 284,541 - 0.223     $ 601,029 - 0.265     $ 683,939 - 0.229
   67,032 - 0.053
  401,414 - 0.315
  335,486 - 0.263
195,926 - 0.086
416,206 - 0.184
386,397 - 0.171
415,226 - 0.139
358,941 - 0.129
 93,292 - 0.031
  780,297 - 0.613     1,256,048 - 0.554     1,717,949 - 0.574
TOTAL
1,062,065 - 1.453     1,868,770 - 1.467     2,855,606 - 1.260     3,269,347 - 1.102
OPERATING
LABOR

OPERATING
MATERIALS

MAINENANCE
LABOR

MAINTENANCE
MATERIALS

LIMESTONE
     1977
DOLLARS-MILLS/KWH


$ 679,628 - 0.313


  253,662 - 0.117


  476,724 - 0.219


1,083,167 - 0.493*


1,202,005 - 0.553
                                         1978
                                   DOLLARS-MILLS/KWH
                           1979
                      DOLLARS-MILLS/KWH
                     1980 (Jan. - June)
                    DOLLARS-MILLS/KWH
$ 755,500 - 0.250     $ 733,016 - 0.485     $ 331,654 - 0.423
  453,140 - 0.150
  414,355 - 0.137
537,172 - 0.355
561,624 - 0.371
  757,951 - 0.251     4,398,066 - 2.90
1,452,792 - 0.482     1,183,169 - 0.782
 69,632 - 0.089
295,094 - 0.376
                    2,399,063 - 3.056
                      289,265 - 0.368
TOTAI
3,695,186 - 1.695     3,833,738-1.270     7,413.,047 - 4.89
                                            3,384,708 - 4.312
 : 6 00,0 00 Pond Dredg J n9

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CATIONS
Calcium  (Ca)
Magnesium  (mg)
Sodium (Na)
Potassium  (K)
          Table 6
LA CYGNE SCRUBBER WATER ANALYSIS
                COOLING            SETTLING
                 LAKE                POND
                126.4               808.0
                 16.3               106.0
                 31.0                52.5
                  5.1                41.6
ANIONS
Bicarbonate Alk  (AS HC03)
Chloride  (CI)
Sulfate  (SO4)
Sulfite  (803)
Silica  (Si02)
                112.2
                 44.9
                295.2
                 * ND
                  1.12
  79.3
 314.0
1995.1
  * ND
  52.0
OTHERS
pH (pH UNITS)                   7.7
Conductivity in Michromhos    820.0
Solids, Suspended               5.0
        Dissolved             610.0
                                      7.5
                                   3500.0
                                      5.0
                                   3450.0
*ND - Not Detected
                              412

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ACKNOWLEDGEMENT
This paper is based upon presentations by:

Mr. C. F.  McDaniel
EPA Symposium on Flue Gas Desulfurization  (1974, 1976,  1977)

and

Mr. Terry Eaton
EPA Symposium on Flue Gas Desulfurization  (1979)
                               413

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                      ONE BUTTON OPERATION
    START-UP OF THE ALABAMA ELECTRIC COOPERATIVE FGD SYSTEM
                         Royce Hutcheson
              Chief Environmental Results Engineer
                  Alabama Electric Cooperative
                         Leroy, Alabama
                         Carl ton Johnson
               Product Sales Manager, FGD Systems
                  Peabody Process Systems, Inc.
                          Stamford, CT
                            ABSTRACT

In September of 1978, Alabama Electric Cooperative started up a
limestone FGD system for its 255 MW Tombigbee Station Unit #2,
Leroy, Alabama.  Since the start-up, the operating experience of
the system has been extremely successful.

A sophisticated control system has been provided for the FGD
system which permits operation from the control room by means of
a single button.  Start-up of the FGD system consisted of pushing
this button.  The unit has been on stream since that time.

The FGD system is designed to remove 85% of the S02 in the flue
gas generator from the combustion of 1.8% coal.  Under performance
test conditions the absorber gas load and inlet S02 content were
20% and 35% respectively greater than design.  Despite the greater
than design conditions a S0£ removal efficiency of 94% was achieved.
A limestone stoichiometry of 1.01 was obtained, probably the lowest
ever achieved in the FGD industry.

After a year of operation, the system has exhibited a high degree of
reliability.  Based upon actual measured hours, the system avail-
ability has been 91.6%.

The FGD system for Unit No. 3, a duplicate of Unit No. 2, has recently
been started up.  Preliminary results indicate similar performance
to that obtained with Unit No. 2.

It is the purpose of this paper to discuss in detail the process
chemistry, system description and controls which have permitted the
successful operation of this unit.
 Preceding page blank
                                 415

-------
INTRODUCTION

Alabama Electric Cooperative's Tombigbee Power  Station
is located on the Tombigbee River approximately 70 miles
due north of Mobile, Alabama.  The most recent  expansion
at this site was the addition of Units No. 2 and No. 3.
Each unit has a rated capacity of 255MW and is  designed
to burn Alabama and Kentucky coals with a maximum sulfur
content of 1.8%.  To meet the emission standard of 1.2 Ibs.
S02 per million BTU, flue gas desulfurization was required.
In September 1975 Peabody Process Systems was awarded a
contract to furnish a limestone FGD system for  both units.

The FGD system for Unit No. 2 was started up in September
1978.  Unit No. 3 was put in service July 1979.  In com-
missioning both units, start-up was achieved by the
pushing of a single button located in the control room.

The pushbutton start-up was simple.  However, the ease
and simplicity of the start-up was not an accident.  It
was the result of careful attention to process  design,
mechanical design and pre-commissioning check out of the
system.  Since the initial pushbutton start-up,  superior
operating results have likewise confirmed the importance
of giving proper attention to these design details.  In
the sections that follow, the details which contributed
to the success of the Alabama Electric Cooperative System
will be discussed as well as the performance history for
both units.
                           416

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SYSTEM DESCRIPTION

The system design criteria are shown in Table No, 1.
                         TABLE NO. 1

DESIGN BASIS PER UNIT
  Unit Generating Capacity              255MW
  Coal Sulfur Content                   1.8% S.
  S02 Emission Standard                 1.2 Ibs, S02/mm BTU
  Flue Gas Volume                       953,000 ACFM
  Percent of Flue Gas Scrubbed          70%
  No, of Absorbers                      2
  No. of Recycle Pumps/Absorbers-        3
  Absorber S02 Removal Efficiency       85
  Alkali                                Limestone
  Waste Solids Disposal Method          Ponding
  Reheat Method                         By-Pass Gas
The flue gas entering the FGD System has been cleaned of
particulate by means of a hot side precipitator,  Two I,D,
fans,  providing the draft for both the boiler, precipitator
and FGD system, are located ahead of the absorbers,  It was
the Owner's preference that two absorbers be used.  Each
absorber has a 22* diameter and is designed for 85% S02 removal,
Seventy percent of the gas is scrubhed and 30% is by-passed for
use as reheat.  Each absorber consists of six spray banks throug;
which a slurry containing calcium sulfite, calcium sulfate and
unreacted limestone is sprayed countercurrent to the gas flow,
The gas, as a result of being contacted with the slurry, is
cleaned of S02=  After leaving the absorption zone, entrained
slurry in the flue gas is removed by means of a two stage mist
elimination section,   The first stage is a weeping sieve tray
deluged with a chemically non-reactive slurry produced by means
°f hydroclones   The hydroclones  are  used to  classify the
                               417

-------
absorber recycle slurry by particle size,   Unreacted limestone
particles are ten CIO) times larger than  the  reacted product,
Hydroclones permit removing the unreacted limestone from the
reacted products because of the particle  size difference.
Decarbonated slurry is used to deluge  the weeping  sieve  tray
and thus prevent a plugging chemical reaction,   Final de-
entrainment, particularly of gas entrained water,  is accomplished
in a second stage which is a Chevron type mist eliminator.  The
clean gas then leaves the absorber where  it is  mixed with by-pass
gas to provide reheat,  At the ductwork juncture where the by-pass
gas and the scrubbed gas meet, a mixing baffle is  used to ensure
a uniform gas temperature prior to entering the stack.

A single limestone preparation system  is  common to both  units.
Limestone rock is crushed on site to approximately a 3/4" size
and stored in a silo.  A weigh feeder  conveys the  limestone to
a ball mill where it is ground to proper  size and  stored in a
tank,  The limestone is fed to the individual units as a 35%
slurry via a recirculation loop.  Limestone slurry is fed to
the individual recycle tanks as required.

Per boiler, both absorbers  are supported  at  grade and share a
common recycle tank.  The recycle slurry  is recirculated from
the recycle tank to each absorber.  Each  absorber  has three
recycle slurry pumps - one pump is dedicated  to two absorber  ,
spray headers,

Waste slurry overflows from the recycle tank  to a  waste  slurry
sump which also collects all drainage  and water used for system
flushing.  The waste slurry is then transported from the sump
to a pond in which the solids are allowed to  settle.   The water
reclaimed from the slurry is recycled  back to the  FGD system
for reuse.   The system operates on a totally  closed loop water
balance basis.  Fresh water is added to the system to make up
for losses resulting from evaporation  and water bound with the
waste solids,
                                418

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FACTORS EFFECTING OPERATING AND MAINTENANCE' COSTS

There are many factors which contribute to the success of an
operating FGD system.  The whole is truly the sum of its parts,
and design detail, no matter, hew small, if ignored can adversely
effect system performance,  The following areas, which will be
discussed, highlight some of the many features applied to
Alabama Electric Cooperative which have contributed to the
FGD System's successful operating experience.

The following factors can and do effect the operability of
an FGD System:

          1.  Absorber design
          2,  Mist eliminator chemistry control
          3.  Simplicity of design
          4,  Materials of construction
          5.  Slurry piping design
          6.  Adaptability to actual  operating conditions

Limestone FGD systems are frequently  approached with the idea
that reacting limestone with S0£ is simple high school chemistry.
This is very far from the truth;  the chemistry is very complex
One of the unique features of this chemistry is that the reaction
products produced can result in significant scaling and plugging
in an absorber.  Consequently, the type of absorber used is
very significant.  Industry experience has shown that in many
systems an absorber with complicated  internals, for example,
tray type absorbers, packed towers, etc,, offer great potential
for solids to deposit     thus hindering the operability of  the
absorber.  For the Alabama FGD system, a spray tower absorber
was used as a basis for the absorber  design,  A significant
feature of the spray tower is that its internals are minimal
and thus minimizes the opportunity for solids to deposit,
Selection of the spray tower design significantly increases
the operability of a FGD system,  However, the mist elimination
section still provides the complicated surfaces which can create
plugging problems.  In any absprber design, de-entrainment is
                                419

-------
a factor which, must be considered to avoid particulate  emission'
through the stack,  A standard design mist eliminator can
provide the opportunity for solids to deposit  on  the  surfaces;.
This is attributed to the fact that entrained  slurry  from  the
absorber zone contains unreacted limestone.  This  unreacted
limestone can then react with the remaining S02 in the  flue
gas and cause solids to deposit on the complex surfaces of
the mist eliminator.  Attempts are frequently  made to avoid this
plugging problem by washing with water.  However,  a system
designed for a closed loop water balance usually  does not  have
the necessary quantity of water available under all load conditions
and all sulfur coals to adequately preclude a  plugging  situation
in the mist eliminator.

An alternate is to control the chemistry by preventing  entrained
limestone from reaching the mist eliminator.   This  is achieved
in the Alabama Electric Cooperative design by  using hydroclones
to remove unreacted limestone from the process slurry and  then
using the limestone free slurry to provide a liquid barrier
below the mist elimination zone,  This liquid  barrier prevents
entrained slurry, with, the unreacted limestone, from  reaching
the critical mist elimination area,  This technique insures
that the mist elimination area operates with, a non-plugging
chemistry regardless of the load or sulfur content  of the  coal
being burned.  It is thus another step in improving the relia-
bility of the system.,

Hydroclones are also used to screen all of the waste  solids
prior to discharge from the system.  This removes  all of the
unreacted limestone from the waste slurry such that the FGD
system efficiency of limestone utilization is  almost  100%

Simplicity of design is another important factor which  adds
to minimal maintenance.  Generally, the fewer  the  number of
components of a system the less the probability of having
problems.   This philosophy has been utilized in the. control
concept for the Alabama Electric Cooperative FGD  System.
Control valves in slurry service, which create both abrasion
                               420

-------
and plugging problems, have been eliminated completely.  The
only exception is a small limestone slurry feed control valve.
The elimination of valves is -made possible by employing gravity
overflow where possible.  An example of this is the main recycle
tank and wash tank.  The quantity of slurry to the spray headers
within the absorber is controlled by turning off pumps rather
than modulating the slurry flow.  This eliminates both a control
valve and the plugging of the slurry pipe line which would occur
under low flow conditions.

In slurry services which require operating over a wide range of
flows, various approaches are taken to prevent plugging of the
slurry pipe lines.

Simplicity of slurry piping design is achieved by having the
absorber recycle slurry pumps feed a dedicated spray header
system.  Thus, two levels of spray banks are dedicated to a
single recycle pump.  Pipe manifolds and isolation valves in
the discharge pipe of the recycle pump are eliminated.  Regu-
lation of slurry flow to the absorber is effected on a step-
wise basis by turning individual pumps on or off as required to
meet emission standards based upon the actual sulfur content of
the coal being burned,  This concept also eliminates plugging
problems due to the creation of dead pockets in slurry pipe
systems and abrasion problems of valves in the discharge piping.

In the limestone feed system, limestone is circulated via a
distribution loop such, that regardless of how much slurry is
required by the FGD system, (Q to 100% of design) the lime-
stone transfer system will always have velocities sufficient
to prevent settling of solids and the resulting plugging which
would ensue.  Likewise, in the waste solids transport system,
a long distance between the absorber and the pond is very common.
This line must also be capable of transporting varying quantities
of waste solids resulting from fluctuating gas load and coal
sulfur content.  A plugging condition resulting from insufficient;
slurry velocities in the waste solids- transport system will
exist when less than design quantities of waste solids are
                               421

-------
produced during normal operation.  An alternate is to design
the system to operate on a constant velocity basis at all
times and thus eliminate the. plugging problem.

As operating conditions vary, the quantity of waste slurry over-
flowing from the recycle tank to the waste slurry sump will like-
wise vary.  Reclaimed water from the pond is added to the waste
slurry sump.  The quantity of water added reflects the difference
between the quantity of waste slurry produced and design capacity
of the system.  This insures that the transfer system has a
slurry velocity sufficient to prevent settling of solids and
prevent plugging under all operating conditions.

The FGD industry has evaluated many materials of construction
with varying degrees of success.  For the Alabama Electric
Cooperative System, linings have been used extensively.

Consider, for example, the materials of construction selected
for the absorber,  All wetted parts of the system are subject
to corrosion,  In addition, the spray absorbtion zone must
contend with abrasion,  To effectively remove the SC>2 from the
gas, all of the gas must be contacted with the slurry.  To
insure proper gas/slurry contacting and prevent short circuiting
of the gas, the spray pattern must be designed such that the
slurry impinges on the absorber wall which creates a sand
blasting situation.  To withstand both the corrosion and the
abrasion, the spray absorber zone has a rubber lining.  The
internal spray headers are carbon steel, rubber lined, rubber
covered, to withstand abrasion internally and externally.  All
connections are flanged and are rubber covered with high alloy
bolting and backup rings to insure that the bolting does not
destroy the integrity of the lining.  Also critical is the
selection of the spray nozzle material which in this case is
a cast silicon carbide,  The nozzle has no internals and has a
minimum opening of 1" which makes it insensitive to plugging
because of trash material in the system,

                                422

-------
In the absorber area above and below the absorption zone,
abrasion is not a problem and only corrosion must be considered.
In these sections, a vinyl ester flake glass lining is used,

Regardless of how good the lining material selected, the liner
is no better than the manner in which it is installed,  Quality
Control during installation becomes critical and directly effects
the maintenance requirements of the system,  Apparently minor
details such as how the rubber lining sections are lapped can
effect the success of the lining installation,  For the Alabama
design, where two dissimilar lining materials are joined, a
full body flange on the absorber module is used to mechanically
join the dissimilar materials.  Though more expensive, the
mechanical joint eliminates the problems associated with chemically
bonding dissimilar materials,  Chemical bonding has generally
proved unsuccessful and will create a maintenance problem,

In any FGD system, the design condition specifications rarely
reflect  the actual operating conditions of the plant.  Sulfur
contents in the coal vary and load conditions vary,  The absorber
design provided has no limitations with regard to minimum gas
flows and yet has the capability of achieving minimum operating
costs by turning off recycle pumps when less than'design sulfur
coals are burned,  This permits achieving  the desired S02 emission
level at the lowest possible operating cost.
                                423

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OPERATING RESULTS

Various concepts have been discussed with, regard to. ensuring
the reliable performance of the Alabama Electric Cooperative .
FGD Systems,  Operating results are the proof as to how success-
ful these concepts have been,  Therefore, it is important to
review actual performance,

In September of 1978, Unit #2 was placed on stream,  In July of
1979 Unit #3 was placed in service.  The operating results which
are discussed here reflect the experience which Alabama Electric
Cooperative has had over more than twenty (20) months of FGD
system operation.

Start-up

The design concept Alabama Electric Cooperative chose for its
control system is a fairly sophisticated one.  By means of
programmable controllers the total start-up and shutdown sequence
of the FGD system is accomplished by the pushing of a single
button,  As part of the start-up, the total system had been
checked out mechanically and electrically such that all sub-
systems were proven,  Having done this, the units were started
up on flue gas by means of pushing that single button,  The
single button start-up was achieved for Unit #2 and duplicated
for Unit #3 ten (10) months later,

The coals which the Tombigbee Station burn are from four or
five different mines located in Alabama and Kentucky.  Though
the maximum design was a 1,8% sulfur coal, the actual sulfur
content of the coals being fired range from 0,88% to 3,6%
Csee Table No,  2),
                                424

-------
PROXIMATE ANALYSIS
MOISTURE %
ASH - 7»
VOLATILE MATTER -
FIXED CARBON - %
SULFUR - %
HEATING VALUE -
BTU/lb,
TABLE NO. 2
TYPICAL COALS BURNED

5.82
13.98
% 31,61
48,60
0,88
11,805

7.40
15,10
31.40
46,11
1.06
11,169

4.64
12.62
35.32
47.42 i
3.62
12,199
The sulfur content variation experienced during the month of
December 1979  can be  considered typical.   This  is  shown in
Figure  No,  1,
                                 Alabama Electric Cooperative
                                     Tombigbee Station
                           Sulfur Content in Coal Burned In December 1979
           I
           S
           1
                                 •  i ^I^^^^^^^^^^^^^^^^^^^^^^^^^^^^T^^^^^^^^^^^^^^^^^^^^^T^^I
                                 10  11 ia U 14 11 16 17 1t 18 20 21 22 23 24 25 2t 27 28 28 30 31
                                      Day of Month
                                        425

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SC>2 Removal and Limestone  Utilization

As indicated earlier,  the  absorbers  had been designed for 85%
S02 removal while burning  a  1,8% sulfur coal,   A limestone
stoichiometry of 1.1Q  moIs of  calcium carbonate/moIs of S02
absorbed had been guaranteed,   Performance tests were performed
by the Owner*s engineers,  Burns & McDonnell,  For Unit #2f a
93,5% 502 removal was  obtained while burning a 2,7% sulfur coal
at an absorber gas flow 24%  greater  than design.   When the test
was repeated for Unit  #3 - a 97% removal efficiency was obtained
while burning a 2% sulfur  coal.   In  both tests, summarized in
Table No. 3, a limestone utilization was very close to the theoreti
quantity, which, reflects 1QQ7»  utilization of the limestone,   This
is attributable to the use of  the hydroclones for removal of
limestone from the waste slurry.	

                           TABIE NO. 3
                    PERFORMANCE  TEST RESULTS
% S in Coal
Gas VolunE/Absorber-ACFM
Inlet S02 Conc,-ppm
Outlet S02 Gonc.-ppm
% S02 Renoval
Limestone Stoichiometry
(moles CaCoo/
moles S02 Absorbed)
Design
Values
1,8
270,000
1106
166
85
1.10

Unit No. 2
Test Value
. 2.7
335,000
1614
105
93,5
1,01

% of Des,
+50%
+24%
+46%




Unit No. 3
Test Value
2.0
270,000
1250
36
97,1
1.02

% of Des.
' +11%
+ 1%
+13%




Power

The power requirements for the  system are low and are summarized
in Table No, 4.  The power consumption shown for the FGD system
under design conditions is less than  1% of rated generating
capacity,  However, the capability of the system to save power
when operating at less than design sulfur coals (1,1% S normal
vs 1,8% S design) is evidenced  by the fact only 0,6% of rated
generating capacity is required,
                                426

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                          TABLE  NO.  4
                 FULL LOAD POWER REQUIREMENTS
                                   Desiga % S Coal       Noimal % S Coal

No.of Absorbers/Unit                       2                   2
No. of Operating Recycle Pumps/Absorbers       3                   1
Power - FGD and I,D,  Fan
     KW Required/Unit                    4275                3496
     % of Rated Capacity                 1,68                1.37
Power - FGD Only*
     KW Required/Unit                    2342                1564
     % of Rated Capacity                 0.92                0.61

*Includes Flue Gas Pressure Drop for FGD System
Manpower

The manpower requirements for the two  operating FGD units
 (total 510 MW) are low -  very low.  Alabama'Electric Cooperative
employs two operators  per shift, on a  four shift basis.  With
regard to maintenance,  all work is performed on a work release
basis.   In terms of maintenance manhours actually expended,  40
hours per week are required for instrumentation and 20-30  hours
per week for mechanical work is required,   These numbers are
 contrary to the 50 or  60  operators which are frequently cited
 for FGD systems.
                                 427

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Availability

Since start-up,  both, units  2 and 3 have  been characterized by-
high, availability.  As illustrated by the graphs shown below
as the  operators learn to run the system properly, the availa-
bility,  improves significantly and availabilities of 9070 or
greater have been consistently achieved.   With the learning
experience having already been gained on Unit #2, start-up of
Unit #3 was virtually trouble free and this is reflected in the
high availabilities achieved right from  the start.  Except for
the  first month of start-up, Unit $3 has consistently achieved
monthly availabilities in excess of 97%,
                            Alabama Electric Cooperative
                               Tombigbee Station
                              Unit No. 2 Availability
                   SOMOJFUAUj  JASONDJ
                            Alabama Electric Cooperative
                              Tomblgbee Station
                             Unit No. 3 Availability
                J*SO*'OJI=MAMJ.IASONO
                                 428

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PROBLEM AREAS

Like any system, problems have been experienced in the operation
of the FGD system.  Fortunately, the problems encountered were
correctable and non-recurrent,

The ball mill system had two problem areas,  A seal at the feed
end of the ball mill had not been installed - this resulted in
leakage of the limestone s-lurry,  Likewise a ball retention helix
at the discharge of the ball mill was not sufficiently deep to
retain large particles.  Peabody corrected both problems and the
system now functions adequately.

No system would be complete without damper problems.  In the
Tombigbee Station these were also encountered,  Double guillotine;
dampers were used in which seal air was injected between damper
                                                    ii
blades.  A spare blower was provided for each seal air system.
When the unit was started up two problems were encountered.  The
operators were undersized and would not move the damper,  When
the dampers were in the open position, flue gas containing 862
would leak into the seal air blower system, condense and create
a corrosion problem.  The operator problem was corrected by
installing larger motors,  The seal air system was corrected by
installing an isolation valve between the blowers and the damper
such, that flue gas would not flow back into the blower system
and condense.  With these problems corrected, the dampers are
operating satisfactorily.

Two problems were encountered in the instrumentation area.  The pH
sensing probe is emersed in the slurry in the absorber recycle tank.
Problems were encountered with slurry leaking into the preamplifier
which caused failure on several occasions.  The preamplifier wa.s
changed to a different type which was enclosed in a seal housing
which prevented leakage.  This eliminated the problem.  Gas flow
measurement by means of an anubar was a total failure.  Under

                               429

-------
Low flow conditions, it was not possible to get a meaningful
signal,  Measurement of gas flow to an absorber was not  critical
and therefore attempts at this measurement were abandoned,

Trash material has caused the spray wash nozzles under the
interface tray to plug.  Placing an in-line strainer in  the
suction of the wash pump which feeds the spray nozzles has
eliminated this problem.

The slurry transfer line from the waste  s-ump to the pond is made
of FRP pipe.   Rupture of this line has occured several times
because of inadequate pipe supports and  also water hammer resulting
from switching waste slurry pumps on and off.  Pipe supports have
been redesigned.  The method of operating the waste slurry pumps'
has been modified by inclusion of a timer to provide a delay
time when switching from an operating waste slurry pump  to a
spare pump,   The object of this is to minimize the effect of
water hammer.
                               430

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SUMMARY OF  OPERATING AND MAINTENANCE EXPERIENCE

The operating experience of Alabama Electric Cooperative has been
unique and  is characterized by:
                    1)  Push button start-up
                    2)  High availability
                    3)  High SC>2 removal efficiency
                    4)  High limestone utilization
                    5)  Low manpower requirements
                    6)  Low maintenance costs
                                  431

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         OPERATION AND MAINTENANCE EXPERIENCE
   OF THE WORLD'S LARGEST SPRAY TOWER SOV SCRUBBERS
                             n	    '••"" " ' •£••••' -•

    :  ROBERT A. HEWITT - TEXAS UTILITIES SERVICES,  INC.
      and A. SALEEM - CHEMICO AIR POLLUTION CONTROL  CORP.
The 750 MW Monticello boiler #3 of Texas Utilities  Services,  fir-
ing lignite coal, is equipped with three large  spray  towers,  de-
signed by Chemico Air Pollution Control Corporation.  Each  spray
tower is sized to handle over one million cubic feet  per minute of
flue gas.  This flue gas desulfurization system uses  pulverized
limestone slurry for scrubbing and includes  a flue  gas bypass as
well as external steam flue gas reheat system.   The FGD system
went into operation in mid 1978 and has since logged  consistently
very high availability as well as high S02 removal  efficiency.
The extreme simplicity of the spray tower system has  resulted in
only modest increase in the power plant's operating and maintenance
staff.  A recent inspection of the system revealed  no major pro-
blems with the tower and duct liners or the  tower internals.   A
few isolated spots on the internal slurry pipes showed wear due to-
close proximity to the sprays.  Failure of the  rubber lining  on
the side mounted agitators and slurry recycle pumps has been  the.
primary source of problems with the system.  The experience with
this system in general has been very satisfactory and Texas Utilitie
has purchased two essentially duplicate systems for the Twin  Oak
Power Station.
Preceding page blank
                              433

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INTRODUCTION

Texas Utilities Company is investor owned  and includes three electi

utilities, two fuel companies, a generating  company,  a service com-

pany and two non-utility companies engaged in energy  related activi

ties.  The total generating capability  at  the end of  1979  was

17,430 megawatts.  Units utilizing Texas lignite as a fuel account

for 5300 megawatts of this capability and  in 1979 about 50% of the
total generation of the system was from the  lignite fired  units.

Monticello #3 is a lignite fired unit rated  at 750 megawatts locatec

at a site near Mt. Pleasant, Texas.  A  typical fuel analysis is

shown in Table I.  Units 1 and 2 were placed in service in 1974 and

1975.  No flue gas desulfurization  (FGD) systems were required for

these units.  Emission regulations applicable to the  #3 unit are a
maximum 2 hour average particulates emission of 0.1 Ibs per 10  BTU,
maximum opacity  of 20% and a maximum 2 hour average  S02 emission of

1.2 Ibs per 106 BTU.

After evaluation of bids Chemico Air Pollution Control Corporation

was awarded a contract to supply the electrostatic precipitators,

I.D. fans and ductwork to the chimney along  with major engineering
and design for the SO2 removal system with an option  of provision jf
the total FGD system.  Included in this contract was  the construc-

tion and operation of a 4000 ACFM pilot plant utilizing flue gas

from one of the existing units.  The objectives of the pilot plant
study were to determine:

     a.  Reactivity of available limestone.

     b.  Optimum stoichiometry, L/G and recycle solids.

     c.  S02 removal efficiency at full and  partial load.

     d.  Limestone consumption.

     e.  Susceptability of system to plugging and scaling.
                              434

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                   TABLE 1
   TEXAS UTILITIES-MONTICELLO NO. 3
TYPICAL LIGNITE FUEL CHARACTERISTICS
      Proximate Analysis-%   Typical     Range
      MOISTURE         32.68    27.5-36.3
      VOLATILE MATTER    30.17    25.0-34.7
      FIXED CARBON      23.88    20.8-27.5
      ASH              13.27     6.4-18.9
      SULFUR            .72     .36-1.79
      BTU AS RECEIVED    6689   6068-7302

-------
In February, 1976 the option  of  having Chemico supply the necessan
additional design, engineering and material for the complete FGD
system was taken.  The  system was  to be completed and ready for
trial operation by January  of 1978.

This FGD system is unique in  that  it involves the world's largest
spray towers.  The system has been in service since August 1978 and
performance and availability  have  been satisfactory.  The main
focus of this paper  is  to review the operating and maintenance ex-
periences to date.

FGD SYSTEM DESCRIPTION
The lignite fired boiler generates about 3.4 million ACFM of flue
gas at full load.  The  FGD  system  is designed to keep the SC>2 emis-
sions to less than 1.2  Ibs/MMBTU.   The S02 removal is accomplished
by scrubbing with an aqueous  slurry of pulverized limestone in
three large spray towers.   The spent slurry containing calcium sul-
fur salts is disposed of in an onsite pond from which the reclaimed
water is recycled to the FGD  system.  A simplified flow diagram of
the FGD system is shown in  Figure  1.  The general arrangement O'l
the major equipment  is  shown  in  Figures 2 and 3.

After passage through the electrostatic precipitators for particu-
late removal, three  centrifugal  boiler I.D. fans drive the flue gas
into a common inlet  manifold  from  which it is equally distributed
into three spray towers for SO-  removal.  The scrubbed gas leaving
the spray towers is  again collected into a common outlet manifold
for discharge into the  stack.

Partial or full bypass  of flue gas around the scrubbers is possible
with two bypass ducts which are  equipped with split louvre dampers
for gas flow control.   The  partial bypass, up to a maximum of 50%,
                               436

-------
                                                FIGURE 1
                      CSWiPLSPlEB FLOW DIAGRAM OF THE FGD SYSTEM
                 AT MONTICELLO #3 BOILER OF TEXAS UTILITIES SERVICE
    SERVICE
    WATER
    BLEED TO
 RETENTION POND
RETENTION
POND WATER
MAKE-UP
    6-
          <>
                       TOP WASH SPRAYS
    BOTTOM WASH SPRAYS
 ~t"\ BLEED
 JJ FROM
    PUMPS
 J-101 B. C. D
                "-©-
                    BLEED
                    SPRAY
                             4"
          RETURN BY PASS
                                      T—TT—I I  I
                                     i  V  I I  I i

                                      ABSORBER
                                       SPRAYS
         GAS OUT


       MIST ELIMINATOR
         TOWER MAKE-UP—'
                                   GAS IN
                                                  12"
	^EMERGENCY
        OVERFLOW
                                                \O

                              "
             PUMP
    J-101A    SUCTION
 RECYCLE PUMP    r~
TO
HEADERS  ^_
  B. C. D
                                                   o
                                                   CO
                                                   CC
                                                   CE
                                                   UJ

                                                   1
                                                                     LIMESTONE SLURRY
                                                                   FROM GRINDING SYSTEM
                                                                      cr
                                                                      01
                                                              y
                                                                                        0-00
                                                                         8"
                                           ^
                         LIMESTONE SLURRY RECYCE
                                 LOOP
                                                                     10"
                                                            LIMESTONE
                                                            SLURRY FEED
                                                            TOR-101
POND WATER
    FOR
   DILUTION
                                                     SEAL POT
                                             R-101
                                             SPRAY TOWER
                                        SUCTION
                                 J-002A            G-003
                            LIMESTONE SLURRY  LIMESTONE SLURRY
                                 PUMP         STORAGE TANK

-------
                                           FIGURE 2
                       GENERAL ARRANGEMENT OF FGD SYSTEM
                   AT MONTSCELLO #3 BOILER SHOWING ELEVATION
                                                                                      CHIMNEY
                                                                     SPRAY TOWERS
                                                                     R-101.201 &301
  PRECIPITATOR
    OUTLET
                                                       INLET & OUTLET
                                                         MANIFOLDS
                                                BY-PAS
                                                 DUCT
                      PRECtFiTATORS
                               FAN ROTOR
                               REMOVAL &
                               ACCESS AISLE
 I.D FANS
K-001 A. BAG
    CO
FROM
AIR PREHEATER
   REHEATER E-001 A & B
REHEATER F.D. FANS K-002 A &
                                      FAN
RECYCLE PUMPS
J-101 A, B. C& D
J-201 A. B. C&D
J-301 A. B, C& D

-------
                                           FIGURE 3
                      GENERAL ARRANGEMENT OF FGD SYSTEM
                  AT MONTICELLO #3 BOSLER SHOWING PLOT PLAN
   '
T
                                                  FAN SUCTION MANIFOLD


                                                           INLET MANIFOLD
                     PRECIPITATOR
                       R-001B
                     PRECIPITATOR
                        R-001A
                                                                  SPRAY TOWERS

                                                                     86'-ir
                                        OUTLET MANIFOLD
     i

.41'-6"  I   47'-6'
                                                  o

                                                  DC
;. CHIMNEY
                                                      i

-------
is automatically controlled  to maintain a predetermined S02 level



in the stack.  The control signal  is  provided by the S02 analyzer



monitoring the stack gas.  A supplemental reheat system is also



provided for use when bypass gas is not sufficient to give the mini



mum superheat of 25°F.  The  supplemental reheat system consists of-



two parallel steam heat exchangers for  heating the ambient air to



300°P which is injected into the outlet duct leading to the stack.



The ambient air is driven by two centrifugal fans.   Model tests for



gas mixing were conducted to determine  the location of bypass con-



necting ducts as well as point of  injection of the supplemental



steam heated air.  The bypass gas  is  injected into breachings of



the outlet manifold while the hot  air is injected through four



opposing ports in the outlet duct  leading to the stack.  (See



Figures 2 and 3).




The SO2 scrubbing is accomplished  by  three self-supporting spray



towers with integral slurry  recycle tanks.   Each tower is equipped



with a single blade guillotine damper on the inlet and a single



louvre damper on the outlet.  The  single louvre damper can be used



for flow balancing if required.  A profile of the spray tower is



shown in Figure 4.  Each tower is  44  feet in diameter in the area



of gas flow and expands to 55 feet to accomodate the recycle tank.



The limestone slurry in the  recycle tank is kept in suspension by



four side mounted agitators.  Each spray tower is equipped with



four spray headers which are fed separately by dedicated centrifuga.



pumps of about 16,000 GPM nominal  capacityc   The slurry in each



tower is sprayed through 200, 3 inch  size hollow cone nozzles made



of silicon carbide.
                               440

-------
                              FIGURE 4
           VERTICAL PROFILE OF THE SPRAY TOWER
           SHOWING MATERIALS OF CONSTRUCTION
                       44'-0" l.D.
                                                GAS
                                               OUTLET
MIST
ELIMINATOR
WASH
SPRAYS
ABSORPTION
SPRAYS
/\ /\ /\
                   /\
x\
b
i
                            x\
                          \ /\ / \ /\
          ACID PROOF
           CEMENT
                                              GAS
                                              INLET
                55'-0" l.D.
                                                     GLASS-FLAKE
                                                     FILLED POLYESTER
                                                     COATING
                                           GRIT-FILLED
                                           FIBERGLASS-REiNFORCEL
                                           POLYESTER COATING
                                                     GLASS-FLAKE
                                                     FILLED POLYESTER
                                                     COATING

-------
Each spray tower has an  integral  four pass,  open louvre vane mist
eliminator which can be  washed  from both sides by spraying makeup
water.  The bottom side  is  continuously washed in sequence by
actuating sprays in 12 pie  shaped segments.   The top is infrequent]
washed in a similar  fashion  as required.   Prior to construction
of the spray towers, gas distribution model  tests had revealed that
resistance imposed by the sprays  was sufficient for uniform gas dis
tribution, hence no additional  gas distribution aids are installed.
Limestone quarry tailings are received by  rail car and stored under
covered shed.  From the  storage pile the limestone is conveyed into
feeder hoppers for the wet  ball mill grinders.  One operating and
one spare mill is provided, each  with a capacity of about 30 tons
per hour with product consistency of 90% minus 200 mesh.  The
ground limestone slurry  is  stored in a day tank and pumped to the
spray towers as required for  pH control in each operating spray
tower.  The pH is automatically controlled by signals from pH meters
sensing the pH of slurry leaving  the recycle tank.
The spent slurry bleed from each  tower, taken under level control,
is disposed of in an on-site  pond.   The reclaimed water from the
dispsoal pond is recycled to  the  FGD system.
The density of the recirculating  slurry is held at 8-10% solids by
the use of nuclear type  density analyzers, which control the amount
of reclaimed water added to the towers.
MATERIALS OF CONSTRUCTION
All equipment and duct work upstream of the  spray tower dealing
with hot gas is carbon steel.   Spray towers  and the  downstream duct
work up to the stack are fabricated from carbon steel which is pro-
tected against corrosion and  erosion by various linings.  Each spray
                              442

-------
tower inlet duct starting from the guillotine damper  and  leading



some distance into the tower is lined with acid proof cement



(Prekrete G8).  The base of the tower up to  the liquid level  is



lined with glass filled polyester  (Ceilcote  103).  Above  the  liquid



level and up to the top spray level  is  lined with  1/8 inch  thick



glass filled polyester lining  (Ceilcrete 2500 AR)  which incorporates



special grit to provide abrasion resistance.  The  remaining portion



of the tower above the top spray level  up to the outlet isolation



damper is glass filled polyester lined.  The ductwork downstream



of the outlet isolation damper, the  outlet manifold and the duct



leading up to the stack are lined with  acid  proof  cement  (Prekrete



G8)..  The slurry recycle pumps and associated piping  are  rubber lined.



The outside of the spray piping inside  the tower is lined with



abrasion resistant polyester lining  (Ceilcrete 2500 AR).  The spr^y



nozzles are made from silicon carbide to provide abrasion proof



service.  The mist eliminator is constructed from  fire retardent



polypropylene and supported on FRP beams.  The support beams  for



the slurry spray piping are rubber lined.  The agitators  for  the .'re-



cycle tank are also rubber lined.




The limestone slurry preparation section is  carbon steel, except



for the ball mills, recycle pumps and piping, cyclone classifiers



and agitators which are rubber lined to guard against abrasion.




The dampers upstream of the spray towers including the bypass louvre



are carbon steel construction.  The  expansion joints  in this  area



are carbon steel and layered asbestos fabric construction.  The



dampers at the outlet of the tower are  316L  stainless steel while



the expansion joints are asbestos filled viton.
                              443

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SYSTEM PERFORMANCE
The FGD system was first placed  in  service on August 18, 1978.
Since that time performance of the  system has been good.  The syste
easily met EPA compliance requirements  during testing conducted
during June, 1979.  The SO, removal efficiency of the towers has
generally been 95% or better.  As a result of this efficiency, it
has been possible to operate through the  unit load range with two
towers under most conditions; utilizing the third tower as a stands
by unit.  However, due to the recycle pump situation, to be discus-
sed later, and the desire to maintain the highest possible compliant
with regulatory agency standards, it has  been necessary to operate
with all three towers in service for the  last year.  This has re-
sulted in satisfactory operation even though two and often three
of the towers have been operated with only two recycle pumps in
service for extended periods.

During the operation of the scrubber to date the sulfur content of
the fuel has varied from 0.4% to 1.7%,  with a typical range of
0.6% to 0.8%.  The E.E.I, availability  of the scrubber has been
99.5% or greater.  Texas Utilities  Generating Company utilizes a
"compliance factor" as a better  indication of the true performance
of an FGD system.  The "compliance  factor" is determined by divid-
ing the number of hours of operation within SO2 compliance limits
by the total hours of generation.   This information is shown in
Figure 6.  The compliance factor reflects non-compliance excursions
resulting from all factors.  The low compliance readings during the
first few months of operation as indicated in Figure 6 resulted
from problems outside of the FGD system primarily related to the
precipitator performance.  Figure 6 also  shows the limitation facto.
which is a measure of generation loss due to FGD system.  During
                              444

-------
                           FOR THE MONTICELLO #3 FGD STSTEM.
            Stofchlometry defined as pound moles of limestone used per pound mole of SO, removed as a
                                       function of recirculating slurry pH.
en

-------
                                                     FIGURES
100
 90
 80
 70
 60
 50
 40
 30
 20
 10
 0

cr
o
o
LLJ
O
_J
Q_
5
O
o
o
CO
LOW COMPLIANCE DUE TO
FACTORS OUTSIDE OF FGD
                                                       ID
                                                       u.
                                                       u.
                                                       O
COMPLIANCE  = HOURS IN COMPLIANCE x 100
  FACTOR      HOURS GENERATOR ON LINE
      SCRUBBER AVAILABILITY FOR 26
        MONTH PERIOD WAS 99.5%
           TIII!TTIII||III|IITTI~~IIIIIIIII
           ASONDIJFMAMJJASONDIJ   FMAMJ  JASO
               1078
                                   1979
                                                             1980
o
o
T~
X
Of
Rf
0
-?
0
^
1
«„¥
I
T^"


90 -

80 -
70 -
60 -
50 -
40 -
30-
20 -

10 -
n -














                                   UJ
                                   -z.
                                   H
                                   U-
                                   LL
                                   O
                                   fc
                                   "Z.
                                                       111
                                                       u.
                                                       O
                                             LIMITATION  ==
                                             FACTOR
                                                              FOH + EFOH
                                                  HOURS GENERATOR ON LINE + FOH + EFOH
                                              FOH  = FULL UNIT OUTAGE ATTRIBUTED TO SCRUBBER
                                              EFOH - EQUIVALENT UNIT OUTAGE ATTRIBUTED TO SCRUBBER
                                                (INCLUDES LOAD CURTAILMENT TO MAINTAIN COMPLIANCE)
            A  s
                                              A  S  r<
                                                        ' T
                                                         n

-------
the 26 month period shown here, the  power generation loss attri-



butable to the FGD system has only been  a  fraction of  a percent-



age.





POWER REQUIREMENTS



Full load auxiliary power consumption of the S02 removal  system



including I.D. fans is approximately 10 MW.  This is based on



the assumption that 35% of the  I.D. fan power consumption is due



to the scrubber operation.  When the limestone grinding system



is in service, the auxiliary load is increased by 0.6  MW.  The



limestone grinding system has had a duty cycle of 5 -  6 hours per



day when the unit is operating  at near full load and the  sulfur



content of fuel is in the range of 0.7 - 0.9%.




REAGENT REQUIREMENTS



The limestone utilization is pH dependent  as shown in  Figure 5.



When the system is operated within a pH  range of 5.5 - 6  the lime-



stone stoichiometry based on absorbed SC>2  is between 1 to 1.10.




MANPOWER REQUIREMENTS



The spray tower system has been relatively easy to operate and



maintain, consequently the manpower requirement for operation has



been modest.  Since the flue gas controls  are intergrated into



the boiler train, the BTG operator can also control the  flue gas



flow to the spray towers.




The following is the list of personnel dedicated to  scrubber



operation:
                              447

-------
     System Area                          Personnel Per  Shift
     Scrubber Control                              1
     Limestone Handling and Milling                1/2
     Chemical Technician                           1/3
     Environment & Instrument Technician           1/4
     Mechanical Maintenance                      1  1/2
     Electrical Maintenance                        1/4
     Total                                       3  5/6

In order to have 24 hour a day seven days a week coverage, a total
manpower of 15-1/3 men is dedicated to the scrubber operation.

OPERATION EXPERIENCE
During the first four months of operation several  breaks in the
fiberglass line that supplies reclaim water from the sludge disposal
pond to the towers were experienced due to poor make-up  of joints
during original installation and vibration due to inadequate support
and restraint of piping in the area.  This has been the  only problem
that resulted in the removal of a scrubber when  the generator was
on the line.  The problem was corrected with the replacement of the
fiberglass line with carbon steel pipe in the areas of failure.

Difficulty has been experienced in moving limestone from the storage
pile to the grinding system due to pluggage of the hoppers and
mechanical failure of the feeders and associated equipment.  Plug-
gage is a problem due to the nature of the limestone used, which
is a by-product of crushed limestone production  and contains a high
percentage of fine material and moisture.  This  results  in pluggage
in the reclaim hoppers especially when wet or when stacked high.
It has been necessary to feed the reclaim hopper with  a  front end
loader.
                              448

-------
Several problems have been experienced with the tower inlet guil-



lotine dampers.  The bottom seals have been damaged due to ash and



sludge accumulation in the seal trough.  Several of the jack screws



and pushrods have been damaged due to binding of the dampers.



Minor linkage problems were experienced on the by-pass dampers;



otherwise the tower outlet and by-pass dampers have performed well.



Since no internal maintenance has been required while the scrubbe.r



has been in service, it is not known whether damper leakage would



permit safe entry while on the line.




Several minor instrumentation problems have been experienced.  Ex-



cessive drift has been a problem with the density control instru-



mentation.  The 0-14 range of the pH instrumentation originally



supplied was too wide to allow good control in the narrow range of



5.6 - 5.8.  The scale was expanded and the pH system has performed



satisfactorily.  The system is easily operated manually with the re-



sult that instrumentation problems have not had any appreciable im-



pact on the operation of the scrubber.




The rubber lining of the side mounted agitator blades has failed



at the tips allowing erosion damage to all agitator blades.




The most significant problem experienced with the FGD system has



been repeated failures of the rubber lining of the slurry recycle



pumps.  Although this problem has not resulted in the loss of avail-



ability of the FGD system or noncompliance with emission limits,



it has resulted in a very significant maintenance expense.  Efforts



are continuing to resolve this problem by reducing the speed of the



pump.  A different manufacturers' pump has also been installed for



testing.




                              449

-------
Another problem was experienced when an  attempt was made  to use



ash water on one tower for mist eliminator wash rather  than fresh



water.  The high levels of calcium sulfate in  this water  resulted



in extreme fouling of the mist eliminator packing material.   The



high velocity of gas through the unplugged areas combined with the



increased load on the other towers resulted  in slurry carryover into



the outlet duct and chimney.



With the exception of the recycle pump problem, the operating ex-



perience with the system has been relatively good.  There have been



no lining problems in the towers.  Spray nozzle plugging  has  not



been a problem and no significant problems have been experienced



with the internal piping other than external erosion due  to  imping-



ment in isolated areas.  It has not yet been necessary  to remove a



tower from service for internal maintenance.



OPERATING AND MAINTENANCE COSTS



Operating and maintenance costs are summarized in Table 2.   Over



the first 22 months of operation the FGD system operating labor



cost has averaged $7,222 per month.  The maintenance material and



labor cost for the scrubber has averaged $65,396 per month with



material only averaging at $35,341.  The maintenance material and



labor cost for the limestone preparation system has averaged



$15,388 per month.



A significant portion (estimated at 40-50%)  of the scrubber  main-



tenance material and labor cost has been due to the recycle  pump



problems.  Resolution of this one problem will significantly .reduce



maintenance cost.
                              450

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                   TABLE 2
 OPERATING AND MAINTENANCE COSTS
   FOR MONT1CELLO #3 FGD SYSTEM
                             Maintenance
                           Labor and Material
Calendar
 Month
A/78
S
O
N
D
J/79
F
M
A
M
J
J
A
S
O
N
D
J/80
F
M
A
M/80
Total
Monthly Average
Scrubber
Operation
$ 7,000*
  7,000*
  7,000*
  7,000*
  7,000*
  7,855
  7,855
  7,855
  7,855
  4,309
  8,028
  6,863
  8,117
  6,890
  7,088
  7,763
  9,695
  7,521
  7,891
  6,695
  7,110
  4.488
158,873
  7,222
Scrubber
Area
$ 5,651
28,085
10,066
12,670
27,307
15,149
24,007
30,730
32,506
78,383
24,597
44,128
60,128
51,222
44,225
127,713
158,096
49,484
119,228
70,494
294,694
130,144
1,438,707
65,396
Limestone
Area
$ 3,598
7,439
5,312
12,351
12,376
10,881
6,703
15,587
9,988
3,821
11,866
19,933
19,147
6,625
17,610
26,351
7,836
12,199
45,223
36,621
15,873
30,185
338,525
15,388
'Estimated Costs
ADDITIONAL ESTIMATED MONTHLY COSTS
   AVERAGED OVEF! 22 MONTH PERIOD
          Chemical Tecnician
          Instrument Technician
          Supervisory
          Total Additional Costs
               1,000
                 500
                 500
               2,000

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             DUAL ALKALI  DEMONSTRATION  PROJECT INTERIM REPORT

                                    by

                              R.  P.  Van Ness
                     Manager of Environmental  Affairs
                       Louisville Gas & Electric Co.
                           Louisville,  Kentucky

                               Norman Kaplan
                Industrial  Environmental  Research Laboratory
                     Office of Research and Development
                      Environmental  Protection Agency
                  Research  Triangle  Park, North Carolina

                                D. A. Watson
                              Project Manager
                            Bechtel  National,  Inc.
                         San Francisco, California
                                  ABSTRACT
This paper will  discuss the results of the recently performed  acceptance
test on the dual  alkali system serving Louisville Gas and Electric  Com-
pany's Cane Run  Unit 6 boiler.  The acceptance test was conducted  to
measure the system performance with respect to the guarantees  offered
Louisville Gas and Electric by Combustion Equipment Associates.  The results
of the testing were as follows:

    •   SO? removal averaged 94% and 143 ppm outlet concentration
    •   Soda ash  consumption averaged 0.042 mole soda ash per
        mole sulfur dioxide removed
    •   Lime consumption averaged 1.04 mole CaO per mole sulfur
        dioxide  removed
    •   Power consumption averaged 1.05% of generation
    •   Filter cake solids averaged 52.2 wt % insoluble solids
    •   There was no net particulate matter addition


Various problems  attributable to the boiler, the FGD system, and the quality
and quantity of  the carbide lime supplied to the system delayed  the accept-
ance testing until  July 1980.  The year-long demonstration period  was  offi-
cially started in May 1980.  The nature of the problems experienced and
their solutions  are discussed.
  Preceding page blank
                                     453

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                                 NOTES
1.   Company Mames and Products

     The mention of company names or products is not to be considered an
     endorsement or recommendation for use by the U.S.  Environmental  Pro-
     tection Agency.

2.   Units of Measure

     EPA policy is to express all  measurements in Agency documents in metric
     units.   When implementing this practice will result in undue cost or
     difficulty in clarity, IERL-RTP provides conversion factors for the
     non-metric units.  Generally, this paper uses British units of measure.

     The following equivalents can be used for conversion to the Metric System:

                   British                    Metric

                   5/9 (°F-32)                °C
                   1 ft0                      0.3048 m
                   1 ft;                      0.0929 nt
                   1 ft*                      0.0283 m3
                   1 grain                    0.0648 gram
                   1 in.                      2.54 cm
                   1 in.;                      6.452 cmi:
                   1 in.-5                      16.39 cm3
                   1 Ib (avoir.)               0.4536 kg
                   1 ton (long)               1.0160 m  tons
                   1 ton (short)               0.9072 m  tons
                   1 gal.                      3.7854 liters
                                      454

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          DUAL ALKALI DEMONSTRATION PROJECT INTERIM REPORT
INTRODUCTION

The Dual Alkali Demonstration Project is a joint effort by a number of
organizations under the sponsorship of the Environmental  Protection
Agency.  The process being demonstrated is a sodium based concentrated
mode using carbide lime as a regenerant.  Louisville Gas and Electric
Company (LG&E) is the owner-operator of the dual alkali system serving
their Cane Run Unit 6 boiler, which is a nominal 280 MW high-sulfur
coal-fired boiler (3.5-4.0% S).  The design was developed by Combustion
Equipment Associates (CEA) and Arthur D. Little, Inc. (ADD.  The system
was erected by the construction department of LG&E under the Guidance of
CEA/ADL at total cost of about $22 million (1976-1980 dollars) or about
$79 per kW installed generating capacity (including waste disposal).

A process flow schematic of the dual alkali process at Cane Run 6 is
depicted in Figure 1.  Flue gas from the boiler passes through the
electrostatic precipitators and is fed to two absorbers.   A recycling
sodium sulfite solution, flowing countercurrent to the flue gas across
two stainless steel perforated plate trays, absorbs SO  according to
the following reaction:

1                  S03=+ S02 + H20 -**2HS03"

In addition, due to the absorption of sulfur trioxide from the gas and
due to the oxidation of sulfite ion in solution, sulfate (S04~) is
formed in the absorbent liquor:
2                  H20 + S03->H2S04-»*2H  + S04

3                  S03= + 1/2 02-*-S04=

The scrubbed flue gas is reheated by combustion gases from a direct oil
fired reheater and is ducted to the stack.

Sodium carbonate is added to either the thickener or the absorber to
make up for losses of sodium in the system.  Bleed streams of the
spent aborbent solution from the absorbers are sent to the regenerator
Reactor trains where carbide lime is added to convert the bisulfite
(HS03~) in the spent absorbent, to sulfite (S03=) in the regenerated
absorbent, precipitating a mixture of calcium sulfite and sulfate
solids:

4                  2HS03" + Ca(OH)2-»*CaS03{ +  S03= + 2H20

5                  S04= + 2HS03' + Ca(OH)2 ->• CaS04| + 2H20 + 2 S03=

The mixed solids actually can be designated as:  x CaS03 . y CaS04 .
z H20 where the ratio x:y is usually greater than 4 and z represents


                                     455

-------
TO ATMOS
                                            FIGURE 1
                                 DUAL ALKALI SYSTEM AT CAME RUN 6

-------
some amount of water of hydration.  No pure gypsum phase is formed.
The sol Ids are separated from the liquor in a thickener and are
removed from the system on washed vacuum filters.  The filter cake is
mixed with fly ash and quicklime in a system designed by I.U. Conversion
Systems.  After fixation the solids are trucked to a landfill site for
disposal.  The clear liquor overflowing from the thickener is returned to
the absorber recycle loop.

A comparison between the design basis and observed operation is given
in Table 1.  The design basis is taken from the design manual produced
under this project, one of the sources of information to which the
reader is referred for additional detail (References 1, 2, and 3).
The system is designed to operate with a liquid to gas ratio of less
than 10 gal./l(r acf including liquor feed to the tray and spray
recycle (typical lime or limestone slurry process are designed for
about 50 gal./10J acf).  The design flue gas pressure drop from the
booster fan to the stack entrance is 8.5 in. of water.

Bechtel National, Inc. is under a separate contract with EPA to provide
an independent test program to assess the operation of the system with
regard to its performance guarantees, and to provide a demonstration
program designed to characterize the system and monitor its performance
over a year-long demonstration period.

Construction was completed in March 1979 and the system was initially
charged and started up in April 1979.  Various problems attributable to
the boiler, the FGD system, and the quality and quantity of lime supplied
to the system delayed the acceptance testing until July 1980.  The year-
long demonstration period officially started in May 1980.  The problems
and solutions are discussed later.

The acceptance test was conducted from July 17 to July 28, 1980. With
one minor exception (filter cake quality), the system proved to be
capable of successfully meeting its performance guarantees.

ACCEPTANCE TEST RESULTS

The 12-day acceptance test was conducted to measure the performance of
the dual alkali system with respect to the guarantees provided to
Louisville Gas and Electric Company by Combustion Equipment Associates.

Seven guarantees concern the operation in the following areas:

        Sulfur dioxide removal
        Carbide lime consumption
        Soda ash consumption
        Particulate matter emissions
        Power consumption
        Filter cake quality
        Year-long system availability
                                     457

-------
                                  TABLE 1
                          Performance Conditions



                                  Design                  Observed

Coal (Dry Basis)

     Sulfur                        5.0% S                   3.7% S (ave.)
     Chloride                      0.04% Cl                 0.02% Cl (ave.)
     Heat Content                  11,000 Btu/lb            10,650 Btu/lb (ave.)


Inlet Gas:

     Flow Rate (Volumetric)        1,065,000 acfm           1,045,000 acfm (max.;
     Temperature                   300°F                    280°F (max.)
     S02                           3471 ppm                 2323 ppm (ave.)
     Oo                            5.7%                     6.7% (ave.)
     Particulate                   0.10 lb/106 Btu          0.84 lb/106 Btu (ave.)


Outlet Gas:

     S0?                           <200 ppm                 143 ppm (ayej
     Particulate                   TJ.10 lb/106 Btu          0.10 lb/106 Btu (ave.)


Boiler Operation:

     Generation                    280 MW                   240 MW (max.)
                                       458

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Table 2 summarizes the guarantees offered and the corresponding results
of the acceptance test.  A brief discussion of each of the guarantee
tests performed during the acceptance test follows.

Sulfur Dioxide Removal

The primary method of determining S02 removal relied on the continuous
Lear Siegler monitor installed in the stack.  This analyzer was certified
in December 1979 by an outside contractor according to the procedure
specified in the Federal Register.  During the acceptance test, as a
backup to the continous monitor and as an ongoing confirmation of the
analyzer accuracy, wet chemical tests of the'stack effluent according to
EPA Method 6 were also performed daily, in conjunction with the particulate
tests.

Preliminary results from the wet chemical analysis showed a discrepancy
between these measurements and the continuous monitor readout.  After
an extensive check of the system, a burned ground wire was discovered
in the signal line of the Lear Siegler continuous S02 monitor.  From
the data on the calibration sequences of the analyzer prior to, during,
and after elimination of the grounding problem, it was concluded that
the signal from the analyzer was offset on the low side by 30 ppm by
the malfunction.  Therefore the continuous stack S02 monitor readings
for the first 7 days of the tests were corrected by 30 ppm.  With
this correction applied-to the early readings, and subsequent to the
repairs to the ground in the analyzer, the two techniques were in good
agreement.

Both measurements showed that the system could meet the 200 ppm S02
outlet concentration guarantee.  Table 3 summarizes the 24-hour average
S02 results for the 12-day acceptance test.  Table 4 summarizes the
simultaneous wet chemical and continuous monitor measurements (the
Method 6 tests were conducted only for the first 10 days).

Lime Consumption Guarantee

The lime consumption guarantee was specified as "not [to] exceed 1.05
moles of available CaO in the lime per mole of S02 removed from the
flue gas".  Lime consumption was determined by analyzing representative
samples of filter cake collected as the cake was discharged from the
filters prior to fixation.  The cake was analyzed for total calcium and
total sulfur.  The total calcium represented the Time used, and the
total sulfur represented S02 removed from the flue gas.  A portion of
the calcium entering the system with the carbide lime is present as
carbonate and therefore does not represent alkalinity available for
regeneration.  Each time the lime day tank was filled, a sample of lime
was analyzed for available alkalinity and total calcium.  From these
results, a correction factor was developed to account for unreactive
calcium in the carbide lime feed.  During the 12-day acceptance test
the calcium consumption, corrected for available alkalinity as described
above, averaged 1.04 moles of available CaO per mole of S02 removed,
thus meeting the guarantee which required less than 1.05 moles/mole of
sulfur removed.  Table 5 summarizes the analyses performed on the filter
cake samples.

                                     459

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                                 TABLE  2
            Performance Guarantees and  Acceptance Test Results
            GUARANTEE
         TEST RESULTS
 S02 Removal

   200 ppm dry basis (D.B.)
   without additional  air dilution
 Calcium Consumption

   1.05 moles available CaO
   per mole S02 removed
 Soda Ash Consumption

   0.045 moles Na2C03 per
   mole S02 removed
 Net Particulate Addition

   Mo net particulate addition
   by FGD system
 Power Consumption

   System will  consume (excluding
   reheat) not more than 1.2% of
   power generated at peak capacity
Filter Cake Properties

  Filter cake will  contain a mini-
  mum of 55 wt % insoluble solids
143 ppm (D.B.) without additional
air dilution
1.04 moles available CaO per
mole S02 removed
0.042 moles Na2C03 per
mole S02 removed
Met particulate removal averaging
88% efficiency
System consumed 1.05% of power
generated
Filter cake averaged 52.2 wt
insoluble solids
                                     460

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                            TABLE 3



            Acceptance Test Continuous S02 Analysis
Acceptance Test
Day
1
2
3
4
5
6
7
8
9
10
11
12
Average
-
24 Hour Continuous S02 Analyzer Results
(ppm, dry basis)
A Inlet
2444
2674
*
*
2265
2567
2113
2116
2395
2372
2292
2167
2340
	
B Inlet
2418
2570
2390
2290
2315
2515
2021
2088
2339
2315
2233
2166
2305
Stack
130
129
130
152
157
140
132
124
146
171
156
130
141
% Removal
94.7
95.0
.94.6
93.4
93.1
94.5
93.6
94.1
93.8
92.7
93.1
94.0
93.9
*  Analyzer printout malfunction
                                   461

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                                     TABLE  4

           Acceptance Test  Continuous Monitor  and  EPA Method 6 Analysis
Acceptance
Day
1
2
3
4
5
6
7
8
9
10
Hours
1400-
1700
1100-
1300
1000-
1300
1200-
1500
1000-
1300
1000-
1300
1600-
1900
1100-
1300
1100-
1400
0900-
1200
S02 Concentration, ppm, dry basis
A Inlet
DuPont
Analyzer
2434
2434
2592
2836
2656
2716
2337
2395
2864
2690
Method 6
2330
2150
2210
2390
2330
2350
2040
2120
2530
2410
B Inlet
DuPont
Analyzer
2516
2423
2670
2674
2606
2418
2250
2330
2721
2624
Method 6
2330
2180
2290
2480
2410
2480
2030
2100
2450
2360
Stack
LSI *
Analyzer
119
122
117
155
136
184
**
113
122
160
Method 6
124
163
154
159
13?
212
137
130
133
137
 *  Analyzer readings for days  1-6  corrected  for the  effect  of  the  burned out
    ground wire
**  Analyzer out of service  for repairs  to  ground wire

                                         462

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                                   TABLE 5
              Acceptance Test Daily Average Filter Cake Analysis


Test Day
1
2
3
4
5
6
7
8
9
10
11
12
Average
As F

Na
wt %
0.55
0.58
0.70
0.48
0.45
1.11
0.58
0.50
1.07
0.45
0.77
0.62

.eceivecTT:

Ca
wt %
14.88
14.60
15.64
15.72
15.15
15.20
14.35
14.44
14.05
14.43
14.85
13.74

lasis
Total
Sulfur
wt %
31.35
31.58
32.60
32.68
31.92
33.20
31.80
32.32
32.58
33.07
33.48
31.64


Insoluble
Solids
wt %
52.65
52.20
52.60
53.72
53.92
51.90
50.70
51.40
51.00
52.43
52.82
50.58
52.16

Mole NaoCO^
Mole S02
0.037
0.038
0.045
0.031
0.029
0.070
0.038
0.032
0.068
0.028
0.047
0.041
0.042

Mole CaO j
Mole S02
1.139
1.109
1.151
1.154
1.139
1.099
1.083
1.072
1.035
1.047
1.064 ;
1.042
1.095
Calcium consumption corrected for available alkalinity (1.095 x 0.95 = 1.040)

*  Correction factor developed from analysis of incoming carbide lime for
   mole of available alkalinity per mole of total calcium
                                        463

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Soda Ash Consumption

The soda ash consumption was determined by analysis of total sodium
and total sulfur in the filter cake.   According to this analysis the
consumption of soda ash averaged 0.042 moles of Ma2C03 per mole of
sulfur dioxide removed and therefore met the guarantee requirement of
0.045.

Particulate Matter Emission

The system was guaranteed not to make any net addition of particulate
matter to the gas stream prior to discharge.  Particulate tests, following
EPA Method 5, were conducted on the inlets to the absorber modules and
in the stack (downstream of reheaters) during the acceptance test.
The results of 10 simultaneous tests showed convincingly that there
was no net addition of particulate matter across the system.  Actually,
the absorber performed as a particulate removal device averaging 88%
net removal of incoming particulate.   Table 6 displays the results
of particulate matter tests performed during the test program.

Although the FGD system met the guarantee requirements, the test was
not very stringent due to the low level of performance by the electro-
static precipitator during the acceptance test period.  The FGD system
was originally designed to process an incoming flue gas stream containing
the equivalent of 0.1 Ib of particulate matter/10" Btu or less.   :
During the acceptance test, however, the level of incoming particulate
matter was almost an order of magnitude higher. Thus it is not surprising
that the absorbers functioned to remove particulate matter even at the
relatively low pressure drop at which they operated.  The particulate
matter emissions from the stack, however, were on the order of 0.1
lb/10  Btu as required for the Cane Run Unit 6 FGD system under the
appropriate requirements to control particulate matter emissions.

Power Consumption

The system, excluding reheat, was guaranteed not to use more than 1.2%
of the total power generated by the boiler/turbine unit at gross peak
load.  During the acceptance test the peak generation was 240 megawatts
(MW).  Correspondingly, the power consumed during peak generation was
2.5 MW, or 1.05%.  The guarantee was met based on peak generation and
also based on average generation over the the test period.  During the
12-day test, the average load was 178 MW and the average power consump-
tion by the FGD system was 2.05 MW, or 1.15%.

Waste Filter Cake Properties

The system was guaranteed to produce a waste filter cake containing a
minimum of 55 wt % insoluble solids.   The filter cake averaged 52.2 wt %
insoluble solids during the acceptance test.  While this fell slightly
                                     464

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                 TABLE 6
Acceptance Test Particulate Test Results
Acceptance Test Day
1
2
3
4
5
6
7
8
9
10
Average
Partlculate (lb/106 Btu)
A Inlet
0.5320
0.6590
0.9470
0.9440
1.1100
0.9900
0.5890
0.6250
0.7890
0.9620
0.8147
B Inlet
0.7120
0.3620
1.0700
0.8060
0.9200
1.4900
0.8470
0.6490
1.2000
0.5930
0.8649
Stack
0.0895
0.0932
0.1110
0.1030
0.1020
0.1020
0.1020
. 0,0893
0.1100
0.1020
0.1004
% Removal
85.6
81.7
89.0
88.2
90.0
91.8
85.6
86.0
88.9
86.9
88.0
                      465

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short of guarantee, the product discharged to the IUCS process was
uniform in moisture content and was suitable for working into a stable
and manageable product through the fixative process.  Optimization of
filter cloth selection and filter cycle will continue with the goal of
showing that compliance with this guarantee can be met during the
demonstration year.

System Availability

System availability, as defined by the Edison Electric Institute (available
hours divided by the total hours in the period under consideration), was
guaranteed to be greater than 90% for the demonstration year.  While it
is too early to report such a figure, through the first 4 months of
the demonstration year (May-August), the availability of the system
has averaged 99.8%.

OPERATING AND MAINTENANCE PROBLEMS

Up to the time of the acceptance testing there were a number of mechanical
problems and a few chemical problems which affected system performance
and led to cumulative delays in executing the program.  None of the
problems have been insurmountable, but their solutions have been
time consuming.  It is important to report the nature of these obstacles
so that future installations of this or similar technology can benefit
from the experience.

Recycle and Thickener Return Pumps

There have been two ma.ior problems with the high-capacity low-speed
pumps for recirculation of absorbent liquor to the trays, and return of
thickener overflow liquor to the absorbers.  The first problem was the
mechanical shearing of the impellers at the hub.  The original pump
impellers were manufactured in two parts: a body and a separate hub for
attachment to the shaft.  The hub was welded to the body.  All of the
impeller failures were on this welded seam.  This problem was elimin-
ated when the pump vendor supplied a one-piece molded impeller body.

The second major problem involved the rapid failure of the suction
side of the pump liner.  As a result of close tolerances between the
casing liner and the impeller, the two surfaces were rubbing; the
resulting abrasion destroyed the liner.  After completely dismantling
the pumps, it was discovered that a finishing step appeared to have
been omitted at the factory, leaving about 1/4-in. excess length on
each shaft.  Milling each shaft to its design size eliminated this
problem.

Mist Eliminator Collapse

Within a few months the startup, both absorber modules experienced
high pressure drop problems.  Inspection of the internal  structure
revealed that the mist eliminator sections had sagged or collapsed
structurally.  The problem was solved by replacing the mist eliminator
sections with those of a different manufacturer.  Since the replacement,


                                     466

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In August 1979, there has been no further problem with the mist
eliminators.

Tray Pluggage

One of the most perplexing problems was the pluggage of the absorber
trays due to deposition.  At first the observed deposit was thought to
be carbonate scale resulting from pH upsets in the modules.  Careful
analysis showed the precipitate to be an aluminum-hydroxy-silicate
complex.  The mechanism of dissolution and subsequent deposition was
traced to the operating pH of the reaction train.  Aluminum was found
to be entering the system with the carbide lime.  At the operating pH
in the reactor, above 11.5, the aluminum compound is soluble in the
liquor.  When the thickener overflow recycle combined with the recircu-
lating absorbent, the resultant drop in pH caused the aluminum to
precipitate on the absorber trays.

Reducing the operating pH of the reactor to between 10.0 and 10.8
reduced the solubility of the aluminum within the reactor and thickener.
This change ahead of the absorber minimized the pluggage problem.  At
the reduced pH set point, however, there is less buffering and control
of reactor pH is more difficult.

Water Balance

The system initially experienced a severe water imbalance.  This was
partly due to a lack of familiarity with the system, and partly because
of low-solids concentration in the carbide lime feed.  The other lime
slurry systems at Cane Run can tolerate an occasional open-loop excursion.
However, the dual alkali process must operate in a closed-loop at all
times, since the high concentration of solubles in the scrubbing liquor
makes disposal unacceptable for both environmental and economic reasons.

The system was designed to accommodate  70% water (30% solids) in the
incoming carbide lime slurry.  Initially the water content was
consistently in the 82-85% range.  At this concentration the system
was receiving twice the design input water flow.  After only a few
hours of operation the volume of water in the system had accumulated to
the point where the lime feed had to be cut off.  The absorbers continued
to function as evaporators until the water level dropped low enough
to resume normal operation.

Strict control of the incoming lime concentration from the supplier and
the addition of a ball mill-hydroclone system to remove oversize particles
alleviated the problem.

Soda Ash Silo Pluggage

Soda ash is added to the system by a dry weigh feeder which feeds dry
solids from a storage silo to a mix tank where it is mixed with absorbent
liquor.  Vented moisture vapor from the hot mix tank backs up into  the
weigh feeder screw conveyor and causes the soda ash to form lumps which
prevent the smooth flow of feed to the system.  The system had a small
fan to blow the moisture-laden air back into the mix tank; however,

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It proved to be under-designed.  Although a larger fan was installed
to improve the situation, the soda ash feed system still remains a
relatively high maintenance item.

Thickener Blockage

In mid-January of 1980, the thickener rake seized during a boiler outage
for repair and ultimately required a shutdown and major overhaul of
the thickener.  This did not occur during normal operation, but rather
during the transient period in which the boiler and FGD were being
shut down for maintenance.  The stoppage was postulated to have resulted
from an overloading of the thickener with washings of accumulated
solids (including fly ash) from the bottom of the absorber.  Lacking a
bottom drawoff, the absorber allowed fly ash to be trapped and accumu-
lated in its lower portion.  The problem could apparently have been
avoided if the solids from the bottom of the absorber had been slowly
pumped to the thickener while the thickener and filters continued in
operation until the absorber bottom was purged of solids.

Correction of the problem took about 3 weeks, during which about 2
million gallons of liquid and solids had to be removed from the thickener
(liquid was temporarily stored, and solids were impounded off site).
To accomplish this, large access entrances were cut in the thickener
sides to allow entry by personnel and equipment to dig out the compacted
solids.

Overloading of the thickener has not recurred.  The solids in the
bottom of the absorbers are still not subjected to mechanical agitation,
but they are no longer washed into the thickener in large slugs.

Sulfur Dioxide Monitoring

Sulfur dioxide measurement in the inlet to and the outlet from the
absorbers is performed by continuous DuPont UV Model 460 SO? analyzers.
In the stack, sulfur dioxide concentration of the scrubbed gas is
measured by a Lear Siegler S02 analyzer.

Three problems have occurred in the measurement of S02 using the DuPont
analyzers supplied with the dual alkali system:

     •   Plugging of the sample probe
     »   Maintaining  a steady calibration of the instruments
     e   Stratification of scrubbed gas across the absorber exit duct

The first two problems have been minimized by daily inspections to
determine if calibration or cleaning of the probes is required.  An
attempt to alleviate the last problem will be made by moving the SO?
probes downstream of the reheaters, which should also help reduce the
first two problems.

Failure of FRP Piping

The FRP (fiberglass reinforced plastic) piping in slurry service (i.e.,


                                    468

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thickener underflow and filter feed) has been a major maintenance Item.
Some failures have been spectacular, some minor.  Late In the fall  of
1979 a flush connection on the underflow line snapped off.  Slurry
from the thickener flooded the access tunnel below the thickener before
the break could be Isolated.  Routinely, elbows In the line from the
thickener to the filter have required repairs because of erosion
damage and failure of the connection bond.  Gradually all the underflow
FRP piping is being replaced with mild steel.  While mild steel  has a
limited life span in this service, failures will be less catastrophic.


pH Control

Reliable and accurate pH measurements for pH control in the reactors
and in the scrubber bleed stream have been particularly bothersome.
The pH related problems are attributed to:

     •  Inability to keep the probes clean
     •  Poor responsiveness of the probes
     •  Pluggage of the sample lines
     •  Poor calibration techniques

Experimentation with different instrument designs and sampling methods
is gradually alleviating the first three problems.  Detailed calibration
instructions and cross checking of the results by two operating departments
have minimized the last.  On-line pH readings are compared daily with
pH measurements taken with a portable pH meter by the LG&E scrubber
laboratory personnel.  If these readings are in disharmony by more
than 0.3 pH units, the on-line probes are recalibrated.

All the original L&N pH probes have been replaced with Great Lakes
models.  To measure the pH of the primary and secondary reactors, a
Great Lakes Model 60 submersible probe is placed in the overflow chute
from primary to secondary reactor, and in the secondary reactor below
the liquid level near the overflow.  The pH of the bleed and thickener
return streams is measured by Great Lakes Model 60 flow-through pH
probes with  ultrasonic cleaners.

Filter Operation

There have been two major concerns with the rotary vacuum drum filters.
First, the cake quality has varied between 45% and 55% solids.  Second,
it has not always been possible to properly wash the cake to meet sodium
consumption guarantee.

Prior to the acceptance test, experimentation with different filter
cloths led to installation of a new filter cloth.  The original cloth
was a polypropylene cloth supplied by National Filter Media of Hamden,
CN.  During the acceptance test this cloth was replaced with a multi-
filament nylon cloth supplied by Thoerner Products Corp., of Pittsburgh,
PA.  The new cloth produced a more consistent quality cake but had a
tendency to blind.  During the acceptance test, cake washing was
sufficient to meet the soda ash consumption guarantee, but the blinding
detrimentally affected the percent solids of the filter cake.  There

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is also some concern that poorer quality solids may be produced in the
reactors at the lower pH levels required to control dissolution of
aluminum and silicon compounds.

Proper cake washing on the filters is subject to a number of considerations.
The wash water rate (as limited by the water balance), the quality of
solids produced, the thickness of the cake (controlled by drum angular
velocity), the wash spray configuration, and the quality of the filter
cloth (blinding characteristics) are all important parameters.  Therefore,
experimentation with different filter cloths and varying operating
parameters is continuing.

DEMONSTRATION PROGRAM PLANS

Although the results reported here have focused on startup and acceptance
testing, it seems appropriate to outline the major work underway and
planned as part of the demonstration program.

Commercial Grade Lime Testing

A month-long test, using commercial-grade lime in place of carbide
lime, will be conducted as part of the demonstration program to confirm
the interchangeability of the two materials for use in a lime dual
alkali system.  The carbide lime contains silicon and aluminum compounds
that are potentially detrimental to the operation of the system, as
previously noted.  Bench-scale tests have already shown that commercial-
grade lime is more reactive than carbide lime, and further improvement
in lime consumption is expected during this test.  Conversely, carbide
lime is thought to contain an oxidation inhibitor not present in commer-
cial lime.  Much of the success of this system relies on the process
liquor remaining subsaturated in calcium sulfate.  During the month-long
test oxidation levels in the system will be closely monitored for any
observed difference in oxidation levels.

Materials Evaluation

Sample coupon racks containing several polymer- or rubber-coated specimens
and various stainless steel coupons have been installed in numerous
locations throughout the system.  Additionally, pipe spool samples
have been installed in the bleed stream and thickener underflow line.
These spools are constructed of various steels with polymer or rubber
linings.

Some of these corrosion samples will be removed after 6 months and
the remainder at the end of 1 year.   Recommendations for materials
for future installations will be based on the analyses of these samples.

Sludge Disposal

A study of the effects of the long term disposal of the sludge generated
by the dual  alkali process has been developed.  For the test program,
unfixed sludge and two different combinations of sludge, fly ash, and
quicklime will  be placed with and without mechanical compaction in six
separate impoundments (each 50 ft x 10 ft x 5 ft deep) for close study.

                                     470

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Test work will include leachate sampling, as well as a number of engineer-
Ing and durability tests to characterize the sludge and sludge-mixture
properties.

Centrifuge Evaluation

Because of the problems associated with operation of the filters in
conjunction with a thickener, a pilot size centrifuge will be installed
in early fall for experimentation.  The centrifuge will be tested to
determine its ability to produce an acceptable waste while separating
sodium compounds from the cake.  It will also be evaluated and compared
with the rotary vacuum filters in terms of reliability and maintenance
requirements.

CONCLUSION TO DATE

As indicated by operation since March 1980, and the successful completion
of the acceptance test in July, the dual alkali process is capable of
achieving greater than 90% SO? removal with an availability of more
than 99% while processing a flue gas generated in a high-sulfur (>3.5%)
coal-fired, full-size (280 MW) utility boiler.  Consumption of raw
materials and power was less than expected (guaranteed) while the S02
removal was over 94% on the average for the 12-day acceptance test.

Most of the problems initially encountered were mechanical and have
been solved or greatly reduced in the operation at Louisville Gas &
Electric's 280 MW Cane Run Unit 6.

Further investigation of filter operation, reactor operation, filter
cloths, materials of construction, and major process component
characterization is underway -
                                      471

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                                 REFERENCES
1.    Van Ness,  R.  P.  et al.,  "Full-Scale  Dual  Alkali  Demonstration  System
     at Louisville Gas and  Electric  Co.  - Final  Design  and System Cost,"
     EPA-600/7-79-221b, NTIS  No.  PB80  146715,  September 1979.
2.   Van Ness,  R.  P-  et al.,  "Project Manual  for Full-Scale Dual  Alkali
     Demonstration at Louisville  Gas  and  Electric Co.  -  Preliminary
     Design and Cost  Estimate," EPA-600/7-78-010, NTIS No.  PB278722,
     January 1978.


3.   Kaplan, N., "Summary of  Dual  Alkali  Systems," in Proceedings:
     Symposium  on  Flue Gas Desulfurization  Las  Vegas,  Nevada,  March  1979,
     Volume II, EPA-600/7-79-167b, NTIS No.  PB80-133176,  July  1979.
                                      472

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        OPERATING EXPERIENCE WITH THE FMC DOUBLE ALKALI  PROCESS

                                   By

       Thomas H.  Durkin, P.E., Plant Manager,  A. B.  Brown Station

                                  and

    James A.  Van  Meter, Director of Power Production and Procurement
               Southern Indiana Gas and Electric Company
                          Evansville, Indiana

                                  and

              L.  Karl Legatski, Manager Process Technology
                            FMC Corporation
                            Itasca, Illinois
This paper reviews the design and initial  operating experience with the
flue gas desulfurization system at Southern Indiana Gas and Electric
Company's (SIGECO's) A. B. Brown Station Unit #1, a 265 MW steam electric
station burning up to 4.5% sulfur coal in a pressurized, pulverized coal
boiler.

After initial  checkout in the spring and summer of 1979, the FGD system
began routine continuous operation.  Overall operating results for sulfur
dioxide collection, chemical  consumption,  availability, maintenance
requirements,  and operating costs are presented.  The problem areas
that contributed significantly to maintenance requirements or non-avail-
ability of the system are discussed in detail.  Not counting the scheduled
outage, the system has enjoyed a 96% availability overall in its first
year of operation on a high sulfur coal  application.  Sulfur dioxide
removal of over 90% has been routinely demonstrated.  Overall operating
costs on an annual revenue requirements  basis are close to the original
projections.
                                       473

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        OPERATING EXPERIENCE WITH THE FMC DOUBLE ALKALI PROCESS
SYSTEM DESCRIPTION

The FGD system at Southern Indiana Gas and Electric Company's (SIGECO)
A. B. Brown Station Unit #1 utilizes FMC's patented concentrated double
alkali process for sulfur dioxide control.  Figure 1 is a schematic
representation of the process.  The central purpose of this paper is a
reliability analysis, for which we have chosen to divide the system
into five major systems, some of which are overlapping:

     A.   Sulfur dioxide absorption
     B.   Lime chemical addition
     C.   Regeneration
     D.   Soda ash chemical addition
     E.   Sludge removal and disposal

Design Criteria

The A. B. Brown Unit #1 is a 265 MW steam electric station burning up
to 4.5 percent sulfur coal in a pressurized, pulverized coal boiler.
Make-up water to the FGD system comes from a collector well located
adjacent to the Ohio River.  Coal is transported to the site by rail car.

For equipment sizing and redundancy purposes the design basis is keyed
to 23,788 m /minute (840,000 acfm) of flue gas at 138°C (280°F) for gas
handling purposes and 85% collection of 9227 kg/hr (20,300 Ib/hr) of sulfur
dioxide for chemcial capacity.

Sulfur Dioxide Absorption

In the double alkali process, sulfur dioxide is absorbed according to
the following reaction:

               Na2S03 + S02 + H20 —> 2NaHS03

          sodium sulfite + sulfur dioxide + water —> sodium bisulfite

An important additional reaction is the oxidation of sodium sulfite:

               Na2S03 + 1/2 02 —> Na2S04

               Sodium sulfite + oxygen —> sodium sulfate

The sulfate ion, which is not active in absorbing sulfur dioxide, can
be partially precipitated by reaction with calcium hydroxide.  The
remaining sodium sulfate is purged from the process through the entrainment
of solution in the dewatered calcium sulfite/sulfate solids sent to the
landfill.

The sulfur dioxide absorption is accomplished in the vendor's
proprietary absorber.   This absorber is designed to allow high sulfur
dioxide collection efficiencies at a relatively low pressure drop without

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                                                 SODIUM MG6ENERATION
                                        ZN»HSOj»CalOH)2-«-C«SO3«
Figure I.  Double Alkoii process schematic including duct arrangement.

-------
 the  use  of  spray  nozzles.  Collection efficiencies above 92 percent
 have been demonstrated while operating at less than 12.7 cm (5 inches)
 of water pressure drop.

 The  pH of the  scrubbing solution is controlled at 6.5.  At this pH,
 the  scrubbing  solution contains equimolar concentrations of sodium
 sulfite  and sodium  bisulfite.  This equimolar solution is highly buffered
 and  can  accept  rapidly changing flue gas inlet conditions caused by swings
 in boiler load  and/or changes in coal composition without upsetting the
 process  control.  As sulfur dioxide is absorbed, the ratio of bisulfite
 to sulfite  increases causing a decrease in pH.  A bleed stream from the
.absorber recirculation loop is directed to the lime reactor, and the
 absorber reservoir  is replenished with regenerated sodium sulfite which
 maintains the  scrubbing solution pH at 6.5.  Maintaining pH levels in a
 range of 6.2 to 6.8 is important for several reasons.  At a pH above 7.0,
 carbon dioxide  absorption becomes significant and can lead to carbonate
 scaling. At a  pH below 6.0, the vapor pressure of sulfur dioxide increases
 dramatically and  can lead to equilibrium-inhibited sulfur dioxide collection.

 Each absorber  is  about 9.14 m (30 feet) in diameter and 21.9 m (72 feet)
 tall  to  the outlet  duct.  Superficial gas velocity is approximately 2.7
 m/sec (9 feet/sec)  at design conditions.  There are three stages of discs
 and  doughnuts  in  each absorber.  A schematic of the absorber internals can
 be seen  in  Figure 1.  The bottom 2 m (7 feet) of the absorber comprise
 an integral  reservoir for the recirculation liquor-  To minimize wet/dry
 interface corrosion problems, the bottom disc and inlet plenum are made
 of Hastelloy G.   The rest of the absorber internals are carbon steel lined
 with a glass flake  polyester resin mastic.  The absorber reservoir is
 additionally lined  with acid resistant brick up to the bottom doughnut for
 thermal  protection  of the lining.  A single stage thermoplastic chevron mist
 eliminator  is  provided downstream of the last absorption stage.

 The  recirculation liquor liquid-to-gas ratio at design condition is
 approximately  1.34  L/m  (10 gallon/1000 ACF).  Recirculation liquor flow
 from the integral reservoir to the top of the last disc is provided by
 a rubber-lined  centrifugal pump, which also provides bleed flow to
 the  lime reactor.

 A small  slipstream  from the recirculation liquor line is passed through
 a pH electrode  to monitor and control recirculation liquor pH by
 controlling the regenerated liquor return flow.  All of the recirculation
 liquor piping  is  fiberglass reinforced polyester for corrosion and abrasion
 resistance.

 One  of the  interesting features of the system is the open bypass
 arrangement in  which the ducting is designed to direct the gas to the
 system booster  fans or through an undampered bypass duct directly to the
 stack.   The advantage of this "open" bypass is threefold.  First, it
 allows upsets in  gas flow through the system to occur without affecting
 the  boiler  draft  controls.  Second, due to the high collection efficiency
 of the absorbers, it allows partial bypass of flue gas while maintaining
 compliance  emissions; this minimizes chemical consumption while providing
 up to 11°C  (20°F) reheat.   Third, gas flow changes can be more readily
 accommodated because of the minimization of the number of dampers.   Each

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absorber module is provided with guillotine isolation dampers in the
inlet and outlet ducts.  A louver damper is provided at the inlet to
each booster fan far gas flow control.  Each booster fan is capable of
providing 14,273 m /minute (504,000 ACFM) at 17.8 cm (7.0 inches) of
water pressure.

Lime Chemical Addition

Two pebble lime storage silos, each 9.14 m  (30 feet) in diameter and
26.5 m (87 feet) tall and fabricated from carbon steel, provide 14
days supply at design conditions.  Pebble lime is transported to the
site by rail or truck.  It is transferred from either storage silo via
a pressure pneumatic system to any of three use bins, one above each
slaker.  Each use bin is fabricated from carbon steel and holds
approximately one-half hour's supply at design use rates.

Regeneration

Calcium sulfite is precipitated by lime addition to regenerate sodium
sulfite for use in the absorber according to the following reaction:

          2NaHS03 + Ca(OH)2 —> CaS03 ' 1/2 H20 + Na2$03 + 1 1/2 H20

                    Sodium bisulfite + calcium hydroxide --->
                    Calcium sulfite + sodium sulfite + water

The regeneration is accomplished in a low-residence-time continuously
stirred tank reactor, which is controlled at a pH of 8.5, the titrametric
endpoint of sodium bisulfite.  The sensitivity of the pH control system
is excellent at this set point resulting in effectively stoichiometric
consumption of lime but a relatively wide control band.

The reactor is agitated with a vertically mounted top entry turbine
agitator.  The lime is fed to the reactor from two paste-type slakers each
capable of feeding nearly 4990 kg (11,000 pounds) of Ca(OH)2 per hour as
approximately a 20 weight percent slurry.  A third installea slaker provides
a 100 percent spare for one of the other two slakers.  Each slaker has an
•integral grit removal chamber.  The reactor is provided with two immersion-
type pH electrodes (one serves as an installed spare) which monitor and
control the lime reactor overflow pH by controlling the feedrate to the
slakers.

The lime reactor overflows to a 30.48 m (100 foot) diameter thickener tank
where gravity settling of the calcium sulfite slurry takes place.  The
thickener concentrates the 1 to 2 weight percent solids in the feed slurry to
20 to 30 weight percent in the thickener underflow.

The regenerated liquor overflow from the thickener flows to the surge
tank by gravity.  Water is added to the tank by level control to
maintain system water balance.  Regenerated liquor is returned to the
absorbers by a centrifugal pump.  There is a 100 percent installed
spare regenerated liquor return pump.
                                        477

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Soda Ash Chemical Addition

Soda ash is stored in a wet system.  It is unloaded from a truck at
a maximum rate of 9072 kg/hr (20,000 Ibs/hr) into a proprietary apparatus
for converting dry soda ash into the monohydrate crystal form in preparation
for use as a saturated solution.  Specifically, saturated soda ash solution
from the tank is sprayed at about 1893 L/min (500 GPM) to wet the incoming
dry soda ash.  The wetted soda ash drops into the tank forming a bed of
sodium carbonate monohydrate crystal in a saturated sodium carbonate solution.
As soda ash solution is used in the process, fresh make-up water is
added to the tank, dissolving the crystal bed to maintain a saturated
solution.  The advantage of using a saturated solution for chemical
make-up is that it allows sodium addition to the absorbers to be controlled
by the volume of saturated liquor delivered to the absorbers because the
concentration is constant.  Soda ash solution from the soda ash storage
tank to the absorbers flows continuously in a loop to minimize concentration
and temperature gradients within the solution layer above the crystal
bed in the storage tank.  This also helps prevent crystallization in the
soda ash transfer lines.  In addition, all soda ash piping is heat
traced and the tank is also provided with steam plate coils in order to
maintain solution temperature.  Flow through the transfer loop and to
the absorbers is provided by one of two centrifugal pumps.

Sludge Dewatering and Disposal

The sludge dewatering equipment consists of three rotary vacuum filters,
each sized for 33 1/3 percent of total capacity required when burning
the maximum sulfur coal (4.5 percent).  When burning the nominal coal
(3.7 percent sulfur) each filter is essentially a 50 percent filter.
Thickener underflow is pumped to the filter vats by an air operated diaphragm
pump.  There are two full flow underflow pumps installed per filter.  The
rotary vacuum filters are primarily of carbon steel construction.  The
filters are knife-discharge type, and the 50 to 60 percent solids cake is
discharged directly into dump trucks for transportation to the on-site
landfill area.  Each filter is equipped with a wash belt compression assembly
for applying wash water to the cake to enhance sodium recovery.

SYSTEM AVAILABILITY

Overall system availability as defined by PEDCO for the first 13 months
of routine operation beginning in Augusts 1979, is summarized in Table 1.
While we feel that the definitions of some of the PEDCO parameters leave
something to be desired from a utility point of view, they at least
provide a consistent basis for comparison.

Table 2 shows the incidents that contributed to system unavailability for
the same period.  The total  scrubber forced outage rate was 3.3%.  At SIGECO,
a forced outage rate for the boiler and turbine of 1% is considered good, and
the goal at A. B. Brown.  There exists here a good comparison of boiler-turbine
to scrubber state-of-the-art design.  Forced outages on the scrubber occur
at a frequency of three plus times what we strive for on the remainder
of the unit.   In addition to the normally scheduled annual outage, we feel
that an additional  outage is required each year for inspection of ducts,
linings and breechings, due to the possibility of corrosion.

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                         TABLE 1  PEDCO INDICES
                         Availability   Operability    Reliability    Utilization
August, 1979
September
October
November
December
January, 1980
February
March
April
May
June
July
August, 1980
 96
 99
 88
 97
 81
 98
 99
 45
100
100
100
 92
 95
 93
 76
 99
 96
 81
 98
 70
 65
100
100
100
 93
 95
 93
 88
 99
 97
 81
 98
 98
 68
100
100
100
 93
 95
93
76
86
88
81
98
69
27
96
83
98
88
95
                   TABLE 2  SOURCES OF UNAVAILBILITY

                   August 1, 1979 to August 31, 1980
Unavailability Cause

Recirculating Pump Failure  (2)*
Miscellaneous Electrical Trips (4)*
Slaker Feeder Controls
Thickener Rake Stall or Overload  (3)*
Isolation Dampers
Lime Reactor Overflow Elbow
Thickener Underflow Pump Suction  Plugged  (2)*
Lime Transfer System Plug-up
Rotary Filters Unavailable
Low Water Pressure
     Subtotal
Scheduled Outages
     Total
                                    Hours
                    Period Hours                       9528
                    Availability                       90.5%
                    Discounting Scheduled Outages      96.7%

 *Denotes number of incidents, if greater than one.
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The following section provides a more detailed chronological discussion
of the incidents that contributed to unavailability.

Month-By-Month Performances

The period of March through July, 1979, constituted the initial check-out
and debugging of the system.  There were some areas which required
modifications for mechanical improvements to cope with situations not
envisioned during the original design phase.  Details on these modifications
were presented in an earlier paper by Durkin et al  (1).

The system availability began to improve dramatically in August as
operator attention and awareness increased and as mechanical problems
became fewer.  The system was down the first day of August for a recirc-
ulation pump impeller lining failure.  The only other system outage was for
the removal of tramp metal from the lime transfer system.  These two
items account for 32 hours of down-time.

September's record shows 48 hours down for an FGD system water filter
tie-in, necessitated by high suspended solids in the service water.
A failure of a 460 volt power cable to one of the recirculation liquor
pumps caused a 600 amp main feeder to overload and trip.  It took only
two hours to reset the feeder and restart all of the systems.  The spare
recirculation liquor pump was put in service and full FGD system operations
resumed.  For two separate periods totalling 51 hours, the FGD system was
bypassed so that precipitator particulate emissions could be tested.
There was one short booster fan trip caused by a mis-wired relay which
was not to be diagnosed until several weeks later.  At the end of the
month, the filter cake quality got so poor that the dump trucks could
not handle it.  We elected to shut down the FGD system so that the filter
building could be cleared of spilled cake.

The filter building clean-up continued into the first day of October.
Again, a short duration booster fan trip occurred.  On October 28, the
FGD system and boiler were taken off-line for a scheduled precipitator
and FGD system inspection.

The inspection outage continued through the first three days of
November.  Once put on-line, the only system outage was due to electrical
problems of the slaker control printed circuit boards.  It took about
12 hours for the cause to be diagnosed and repairs made.

The most significant outage occurred in December.  After a short duration
boiler trip, the thickener rake was discovered to be stopped.  Numerous
attempts were made to restart the rake to no avail.  Finally, the thickener
had to be drained and the solids removed to free the rake.  The system
outage lasted 146 hours.

January's record shows only 12 hours of downtime.  The thickener rake
torque instruments indicated a steady increase almost to the point of
motor overload.   Since we were fearful of another stall, the system was
shut down.   After several hours of filtering, the torque dropped and the
system put  back  on line.
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We experienced a period of poor quality filter cake in February, similar
to September's situation.  We elected to take the FGD system off-line
for building and roadway clean-up.

March downtime was split between two outages on the balance of plant
and the completion of roadway work begun in February.  Availability was
45% based on 444 boiler hours.

May downtime was due to an outage on the make-up water line to the cooling
tower during which some internal scrubber inspection work was done.

July downtime was caused by two scrubber recirculating pump impeller liner
failures in three days.

August downtime was caused by pluggage of the thickener underflow pump
suction header, and a couple of other minor problems.

Overall, since the FGD system reached stable operation early in August
of 1979, it has operated at 90% availability and a 3.3% forced outage
rate.  The FGD system's longest continuous run has been 54 days, and it
had run 71 days between partial forced outages.

RELIABILITY ANALYSIS

While the total availability record at A. B. Brown has been good compared
to most other FGD systems now in operation, our goal is to achieve a
forced outage rate of 1%.  To better understand how we can improve our
availability in this and future installations, we have performed a
reliability analysis on each of the five major systems described in
the first section of this paper.  The systems are not mutually exclusive,
meaning that an element may be included in more than one system.  The
thickener tank is an example, since it is included in both the regeneration
system and the sludge removal system.  Also, the systems do not necessarily
follow the flow of one fluid, but generally follow the series of events or
reactions that must occur to insure availability and compliance.

Figure 2 shows the block diagram of the five systems.  All of these
systems are integral to scrubber availability and the failure of any
system will result in scrubber downtime.  Reduced capacity of a system
may-result in unavailability, but most likely will be considered available
at low load. With a total FGD system availability of 96%, shown at the far
right side of Figure 2 the contribution of each system is shown in the
.lower right hand corner of each box.  The decimal1 in the lower left hand
corner is the sizing of each part, compared to the boiler full load gas
flow or maximum sulfur dioxide collection.

Sulfur Dioxide Absorption (A)

Figure 3 illustrates the elements of the sulfur dioxide absorption system.
The gas contact systems have performed at a reasonable level of reliability,
99% plus, but not without some problems.  The absorbers have operated
perfectly, with no pluggage and only minimal lining deterioration.  The
single stage chevron type mist eliminator has given us some problems.  In
                                       481

-------
00
ro
             3000 PPM
               302
          FROM BOILER
          SLUDGE REMOVAL
           AND DISPOSAL
          1.0    "E"  97%
         CHEMICAL ADDITION
           SODA ASH"D"
         1.0         100%,
             3000 PPM
               S02
           FROM BOILER
 GAS CONTACT NORTH
                                         0.6*
              99%
                    400 PPM
  REGENERATION
        "c"
1.0
98%
                                          CHEMICAL ADDITION
     LIME "B"
1.0
99%
                                         GAS CONTACT SOUTH
                                                 "A"
0.6
99%
400PPM SO?,
                                        GAS TO STACK
                                             96%
                                                             * DENOTES SUBSYSTEM FRACTION OF
                                                               TOTAL SYSTEM DESIGN CAPACITY.
                        Figure 2.  Reliability Block Diagram of FGD major systems.

-------
oo
OJ
                                                                                  TO  SYSTEM V
                                                                                   REGENERATION
                                                    RECIRC.
                                                     PUMP
                                                  0.6   98%
                                                                                      SCRUBBED GAS
                                                                                        TO  STACK
                                                                                       SYSTEM "A"
                                                                                     99 % AVAILABLE
  BOOSTER
    FAN
ABSORBER

0.6  IOO%
CONTROL
 VALVES
 GAS FROM
PRECIPiTATO
                                                    RECIRC.
                                                    PUMP
                                                  0.6  98%
              FROM SYSTEM  D"
                                 iSOLATION
                                  DAMPER
             SODA ASH ADDITION
                                                    QUENCH
                                                    SPRAY
FROM  SYSTEM V
                   REGENERATION
                                                   0.6  100%
                                       System MA\ gas e©rstaet (ont sids only)

-------
June of this year, recirculating liquor pumps in the south module began
to fail at an alarming rate.  Cavitation was the suspected problem,
caused by pluggage of the pump suction.  Inspection revealed that two
sections of the mist eliminator had collapsed into the scrubber sump,
blocking the suction pipe.  The mist eliminator sections appeared to slip
off the 7.5 cm (3 in) wide shelf supporting them, and the Inconel tie-wires
were not adequate to hold them.

The mist eliminators seem to perform adequately when in place.  However,
in recent months there has been evidence of increasing losses of sodium
due to entrapment.  The problem appears to coincide with the collapse of
several sections of the mist eliminator.  The losses are primarily in the
form of high sodium levels in the drainage from the stack.  Sodium levels in
the exit gas, as determined by analysis of EPA Method 5 particulate catches,
have been consistently low, in the range of 0.005 to 0.006 Ib/mm BTU, or
about 10% to 15% of the total particulate.  This suggests that the entrained
drops are large enough that they fall  down the stack.  Stack drain losses of
sodium may amount to 1 to 2% of the SOp collected, or up to more than
one-half of the total excess sodium consumption, which will be discussed  in
more detail in a later section.  Steps are now being taken to repair the
existing mist eliminator and add a second level  of eliminators to reduce
losses.

The rubber-lined recirculating liquor  pumps have performed about  as
expected.  During engineering, pump lining and impeller life were
estimated at one year and the pumps were spared accordingly.  Disregarding
cavitation problems and some sub-par work on original installation, our
experience has been reasonable.

The system design calls for three levels of protection for the scrubber
lining:  1)  cooling with recirculated liquor with the recirculation
pumps; 2)  isolation dampers; 3)  water quenching of inlet gas.   Plant
experience with the guillotine isolation dampers has been poor.   Original
materials of construction caused some  problems,  and of late, seemingly
minor problems such as a stuck relay in the entry door logic have led
to major problems.  In addition, the lead time for fabricated pieces
of a material suitable for a wet flue  gas environment is truly ridiculous.
As a result, the plant relies on water quenching of the incoming  gas to
protect scrubber internals more than we rely on dampers.

The outlet duct from the absorber to the outlet isolation damper is
coated with a flake glass lining.  In  the outlet duct from the damper to
the stack, which is lined with an epoxy vinyl  ester coating, the lining
has failed dramatically on one module, subjecting the carbon steel structure
to severe corrosion.  This duct segment is exposed to cool 54°C  (130°F)
saturated gas when the scrubber is in  service and to hot 149°C (300°F) gas
those few times it is off.  An appropriate low carbon, high molybdenum
stainless steel will be installed at the next scheduled outage as a
replacement of the corroded duct.  The corresponding duct segment on the
other module will  be lined with a new  experimental lining we want to try.
This duct section was patched from the outside with the unit on  line, and
has caused no downtime.
                                       484

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Lime Chemical  Addition (B)

The lime chemical addition system shown in Figure 4 has been responsible
for less than 1% of tne FGD system 3.3% forced outage rate, but this 99%
availability is not an accurate measure of the strength of the design and
operating capabilities of this system.  There have been numerous instances
of reduced capacity because of inadequate lime supply to regeneration.
However, the surge capacity of the thickener tank has helped us minimize
any lost time or non-compliance.  The system can run for several hours
before a reduction in scrubbing capacity, due to the storage of 3,028
kiloliters (800,000 gallons)  of regenerated liquor in the thickener.
Circulating low pH (6.5) liquor through unlined carbon steel piping
and tanks does cause some accelerated corrosion and at every outage great
care is taken to ascertain material integrity with a view toward possible
future replacement.   To date, no problems have been seen, but we are
installing additional monitors to record the pH in these unprotected
areas.  As our experience grows, we will be establishing some lower range
cutoff points below which we will not operate, based on engineering
judgments.

Interruptions in lime supply are caused by failure of the lime transfer
system or by foreign material in the lime.  The transfer system itself,
while it has performed reasonably well, is recognized by plant personnel
as a weak link.  The system has only one blower and one feed line going
from the two storage silos to the slaker use bins.  A malfunction of
any one component will shut down the entire system, and result in low
pH incidents described previously.  We are engineering some redundancy
for lime transfer to the slakers.  As a system, lime transfer has been
only 98.5% available.

Regeneration (C)

The second largest cause of scrubber forced outages is the regeneration
system.  Figure 5 shows the elements of the system.  Slakers are Included
in both system B, lime addition, and C, regeneration.  The regeneration
area has not caused much downtime on the scrubber, but as with the lime
addition system that is not a fair measure of how well it performed.
Our incidence of reduced capacity due to regeneration problems has been
significant.

As designed, pH at the lime reactor discharge is fed back to the slaker
feeder controls to control lime addition.  The pH normally swings plus
or minus one unit from the setpoint.  The control problems in this
situation are obvious.  As a result, slaker feeders are constantly
varying in response to both load changes and normal swings.  This causes
greater than normal wear on the rotary air lock feeders, and they overcharge
the slakers occasionally, causing plug-ups.  Our early experience with
lime feeder controls was very poor.  Slaker control problems are often
attributable to the dusty, wet environment of the slaker building.
All local  control panels are mounted adjacent to the slakers, and subjected
to the same ravages of steam, caustic, and water as the slaker itself.
NEMA dustproof rated enclosures have brought these problems to a manageable
level.
                                       485

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00
o>

UNLOADING a
STORAGE
1.0 100%


«fr
pt


LIME
TRAfdCFfrp
1.0 94%

tot
p


WATER
ClBppJ V
1.0 99%



|->
... fih
IF
- feft

SLAKER 1
0.5 94%

SLAKER 2
0.5 94%

SLAKER 3
0.5 94%
                      Figure 4.   System  B , lime  chemical  addition

-------
 SLAKER I
0.5   94%
 SLAKER 2
0.5  94%
 SLAKER 3

0.5   94%
SYSTEM "A"- NORTH
  BLEED VALVE
  0.6      99%
                    LIME
                   REACTOR

                  1.0   99%
SYSTEM "A"- NORTH
  BLEED VALVE

  0,6     99%
pH CONTROL


1.0   99%
                REGENERATION
                                        SUR6E


                                     1.0   100%
                                  THICKENER


                                  1.0   98%
    Figure 5.   System "C",

-------
The lime reactor overflow elbow has been patched several times and is
scheduled for replacement in the near future.  Failure analysis questioned
the suitability of carbon steel in a service where it is exposed to
abrasion from lime grit and corrosion from occasional pH excurisons.

The remainder of the regeneration system has operated well with minimal
problems, and has offered the level of reliability that is expected
from power plant machinery.

Soda Ash Chemical Addition (D)

The soda ash chemical addition system shown in Figure 6 has not contributed
to any FGD system downtime, although low sodium concentration in the system
has resulted in some non-compliance.  This is not seen as a problem though,
and with fourteen days' inventory available 1n the tank, no changes are
foreseen*

Sludge Removal and Disposal (E)

As shown in Figure 2, the sludge removal and disposal system has been the
weakest of the five systems, due to;both mechanical  and process difficulties.
This weakness would be even more costly in terms of availability if the
system did not have some surge capacity in the thickener tank, which allows
the plant to run as long as eight hours at full load without filtering.
However, this is not a preferred operating mode, and it is not without
some detrimental system effects, so in deciding to utilize the thickener
surge capacity the value versus the consequences of continued operation
must be carefully considered.

The detrimental  side effects of utilizing the thickener surge capacity
are as follows.   First, as part of our filter cake quality testing, it
was shown that increasing the inventory of solids in the thickener tanks
tends to increase the pH of the underflow, apparently due to the continuing
reaction of small amounts of alkali.  This increase in underflow slurry
pH coincides with a deterioration in cake quality.  Second, the thickener
is designed with a pivoted rake and no powered rake lifting mechanism.
The rake and drive are protected from overload by a spring loaded clutch,
designed to trip the rake drive when it reaches its torque rating.  If
the rake were to trip with a high inventory of solids in the tank, it
would sink into the mud and be impossible to restart.  This would require
a lengthy outage to pump out the thickener tank with the loss of $50,000
to $100,000 worth of chemicals.  Third, operation of the gas contact system
without filtering will increase the total volume of material -- solids
and liquids -- in the thickener tank and result in liquid losses because
of overflowing the surge tank capacity.  This costs money in chemical
losses, amounting to 10 to 20% of the excess sodium consumption.

Figure 7 shows in greater detail the reliability analysis of the sludge
removal and disposal system, and shows elemental availabilities much lower
than the 97% for the system.  Redundancy is the key, along with high
maintenance requirements and quick response to problems.  Availabilities
of the filters have been in the mid eighties, but the problems have been
generally unrelated to design.  Rotary vacuum filters are high maintenance
                                       488

-------
&
pp
SLUR-0-LYZER
TANK
1.0 100%
fe,.
i
k r
TRANSFER
PUMP i
1.0 !00%
tot
t*
PIPING LOOP
8 HEAT TRACE
1.0 100%
£


1.0
!00%

TRANSFER
PUMP 2
1.0 100%


                          Figure 6. System UD",
Soda ash chemical addition.

-------
•JD
O
                                            PUMP  H

                                            0.5 80%
                                                                                TRUCK I

                                                                               0.3  50%
0.5  88%
                  THICKENER
     FROM  LIM
      REACTOR
                                                                               0.3  50%
                            SURGE
                           CAPACITY
                           1.0  8 HRS.
                                                                               TRUCK 5

                                                                               0.3  50%
                                                                                        HAUL ROAO
                                                                                      TO LANDFILL
                                                                                       SYSTEM V
                                                                                      % AVAILABLE/
                         Figure  7.    System  E , sludge removal  and  disposal

-------
items.   Cloth life is only one to three months, and between cloth changes,
maintenance is required regularly to keep caulking ropes in place and to
repair  holes in the cloth.  A large portion of our filter problems concern
the vacuum pumps and filtrate return pumps becoming overloaded with solids
earned over from the filter, generally through holes in the cloth.  The
solids  appear to be mainly grit discharged from the slakers.  The lime
supply  at 88% - 90% available CaO, has a reasonably high amount of grit which,
no doubt, contributes to this condition.

Another problem area is the underflow pumps, which have had only 80%
availability.  Here the problems are basically design related.  The pumps
are air operated double diaphragm type.  Air supply to the pumps is
controlled by the filter vat liquid level.  As vat level drops, the
pumps are energized to refill vat level.  This constant on-off operation
allows  the pump, the suction lines, and the discharge lines to lie full
of thickener underflow slurry.  They will eventually clog.   Various
operating procedures to flush the system on startup and shutdown have
lessened the problem but not eliminated it.  It appears that any design with
low or  intermittent flow in this critical area is a weak one.

The final element in the sludge removal and disposal system is the trucks.
A. B. Brown is using tandem axle dump trucks to transport filter cake
to the  landfill.  Two to four trucks are required for full load operation
depending on the combination of filters in service.  Our experience has
been very poor in this area.  With five trucks assigned to filter cake hauling,
we have had three or more available for load only 75% of the time.  This
is another area where the surge capacity of the system comes into effect.
It gives us enough time to repair either the right combination of filters or
trucks  to maintain availability and compliance.

Truck problems have been in two general areas:  drive train (transmission
and axles) and tailgate.  Both of these are contributed to very heavily by
the condition of the sludge.  Wet, soupy material is not only hard to
handle  in the landfill but exceptionally hard to drive through, and it
exerts  a great deal of hydraulic pressure on the tailgates.

Trucks  frequently must be taken out of service to clean beds.  This
situation occurs not just in winter when cold weather causes some freezing
to beds, but also during hot weather.  We have experimented with plastic
liners  and feel that they are an improvement but not a cure-all.  Many
of our  truck problems could probably be solved with more suitable trucks.
However, the existing filter building layout limits our choices.

In addition to the mechanical aspects of the sludge removal system
performance, there are process considerations.  There have been extreme
variations in cake quality that are not entirely due to mechanical
conditions.  While difficult to quantify, it is clear that poor cake
quality increases the cost of operation and maintenance and negatively
impacts availability.

A large effort in the last six months has been devoted to understanding the
variations in quality, and while we're not completely satisfied that we
understand what's happening, we have found some general truths.  First,
                                       491

-------
it Is clear that cake quality is directly related to crystal size and
shape; moisture content is not so important, i  Second, as noted above,
elevated pH generally deteriorates cake quality, at least in this application.
Third, transient process conditions are bad; our worst cake has always
been associated with situations in which we changed solution chemical
composition rapidly.

Finally; we believe there is a relationship between sodium sulfate
concentration and cake quality.  Sodium sulfate concentration seems to
affect the size and shape of the calcium sulfite crystals formed in the
regeneration section.  All other things being  equal, the greater the
sulfate concentration the larger the size and  the more irregular the
surface of the crystal, as shown in Figure 8..  Crystals with an irregular
porcupine-like surface are called radial crystals.  The larger, more
radial crystals result in a filter cake with better handling properties.
As noted earlier, sodium sulfate formed in the system is purged from the
process through the entrainment of solution in the dewatered filter
cake.  Since the fuel sulfur level is high, there is a large amount of
cake formed in this system.  This means that the concentration of sodium
sulfate in the scrubbing solution does not need to be very high to
maintain equilibrium in the system.  (The amount of sulfate formed is
relatively fixed for a given load.  Thus, the  more cake formed the lower
the concentration of sulfate in the cake.)  The situation is aggravated
by transient losses of sodium sulfate through  carryover into the gas
stream or spills.

There are three general categories of sodium loss to consider: entrainment,
filter cake, and miscellaneous spills and leaks.  Entrainment, or stack
losses, was discussed earlier, and we hope to  correct that problem during
our next outage.  Filter cake washing, while steadily improving, is still
not up to design.  We plan to increase our hot water capacity in the FGD
area in an attempt to improve our washing.  Spills, a problem in early
operation, have been brought under control in  recent months, but we still
are considering increasing our surge tank capacity to allow for greater
fluctuations in the water balance.  We are hopeful, but still not certain,
that these improvements will allow us to simultaneously reduce sodium
consumption and improve cake quality.

While we endeavor increasingly to implement the above improvements in
our routine operation, there are aspects of cake quality that we still
do not understand to our satisfactaion.  Continuing research projects
at FMC's Central Engineering Laboratories and  Purdue University, together
with experiments at A. B. Brown, will hopefully eventually lead to a
scheme for consistent production of easily handleable cake and a better
fundamental understanding of the numerous parameters that effect the cake
quality.

Conclusion

Typically, in the operating life of mechanical equipment, there is a
break-in time during which breakdowns are frequent; a useful operating
life during which breakdowns are at a low, manageable level; and finally
a wear-out period when failures increase dramatically.  Without changes
                                       492

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ZOOOx, low sulfate
10,000x, "low sulfate
2000x,  medium sulfate
10,000x, medium sulfate
2000x, high sulfate"
 105000x, high sulfate
Figure 8.  Effect of  increasing  sulfate concentration on crystal structure.




                                     493

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and improvements, we feel  that the availability of the equipment has
reached its high point.  With that in mind and remembering that our
scrubber forced outage rate is three plus times what we would like, we
are engineering system improvements in these areas:

     1.   Filter cake quality
     2.   Underflow pump recirculation
     3.   Duplicate lime transfer system
     4.   pH controls

We hope that these improvements will affect the wear-out period and
allow us to improve our availability.  Some other problem areas addressed
in this paper are locked into the system because of original  design,
layout, or available space.  Frankly, we feel  that it is unrealistic to
expect the first utility installation of a new FGD technology,  even
with the process advantages of double alkali,  could ever achieve the level
of reliability and availability that the balance of the system  achieves.
However, we feel that the problems we have had are primarily  mechanical,
and correctable, in future installations.

OPERATING COSTS

The variables in the FGD system operating costs are:   operating manpower,
maintenance expenses (labor and materials), lime usage, soda  ash usage,
power and landfill costs.   In analyzing these  costs  for equation back
to the manufacturer's original estimate, upon  which  the selection of the
double alkali scrubber over a lime or limestone system was based, several
adjustment factors must be applied to the costs incurred in order to
put them on the same basis as the specification and  proposal.

The system is designed to handle 265 MW gross  of flue gas at  143°C (290°F)
and 5.0% Op.  Coal burned was to be a maximum  of 4.5% sulfur, 26,749,000
joules per kilogram (11500 Btu per pound) and  0.05% chlorides.   Cost analysis
was based on 70% load factor.   Actual experience has been off-evaluation
on some key items:  sulfur has averaged much closer to 3.5%;  the unit load
factor has been 58% rather than 70%; and the flue gas volume  and excess
air have been higher than anticipated.  All these items significantly impact
the cost comparison of actual to guarantee.  Rather than go through a
laborious explanation of each variable with all applicable adjustments, it
is most likely more informative to qualify each.

Operating manpower was based on one additional man per shift.   Our
experience has been very favorable in this area.  In all but  extremely
unusual circumstances, one local FGD system operator has been sufficient
to operate all equipment.   The scrubber control board is located in the
main control room, adjacent to the boiler-turbine-generator control panel,
and this design feature has been a big manpower saver.  Existing control
room personnel operate the panel.

Maintenance costs (including electrical and instrument) were  predicted
to be 1.5% of capital  costs per year.  Both labor and material  were
included in the 1.5% figure.  Our experience has shown this to  be low
by about 50% after allowing for inflation.  Future maintenance  costs
                                       494

-------
are expected to increase as we approach the "wear out" period on some of
our major pieces of equipment.  The  1.5% maintenance was a concession
made during bid analysis to the claimed features of the double alkali
process versus 2.5% of capital for lime systems and 4.0% of capital for
limestone systems.  While our experience has not been quite that good,
experience by others would indicate that our predictions for lime and
limestone were also low.

Excess lime usage was predicted to be 1% or less (stoichiometric ratio -l.Oi;,
Our experience has shown excess lime usage as low as 0.02% (stoichiometric
ratio = 1.002) to be attainable under normal operating conditions.

Soda ash usage was predicted to be 2.5% of the moles of S0? collected
plus 1% allowance for the chlorides in the coal.  As alreaay discussed,
our usage has been higher than expected and the increase over design has
been attributed by FMC to inability to wash the filter cake with adequate
amounts of hot water and to system losses through spills and stack drainage.
It is anticipated that improvements in soda ash usage will be made.  Soda
ash prices have jumped sharply in the past year, and the price now is
almost double what was budgeted in 1976.  However, soda ash is not a
large percentage of total operating cost and we are hopeful that recent
price increases, which were caused by some unexpected closings of obsolete
synthetic soda ash plants, will not recur.

Power requirements were predicted to be about 0.8% of net generation
at full load.  Our experience has been favorable in this area, with the
FGD system using slightly less than the predicted amount.

Landfill costs were predicted at $2.00 per ton of material.  Our experience
to date with the landfill operation has not met our expectations.  The
double alkali filter cake has generally been of a poorer quality than we
anticipated, contributing to the problems and expense at the landfill.
The two dollars per ton (1977 dollars) would nave been adequate were it
not for the difficulties resulting from the cake quality.

The double alkali system was purchased based on a lower evaluated cost.
In cents per kilowatt hour, FMC's process was estimated to cost 0.269
vs. 0.306 for the next closest system, as reported by Wagner (2).  Applying
all appropriate correction factors to our experience, and inflating the
other systems costs by actual reagent costs and the consumer price index
for other items, the FMC process still exhibits the lowest cost for this
installation, although not by as wide a margin.

CONCLUSION

In conclusion, SIGECO feels that the Double Alkali System installed at
the A. B. Brown station can be successfully operated by utility personnel
and can meet the requirements of Federal New Source Performance Standards
while burning high sulfur midwestern coal.
                                       495

-------
                               REFERENCES
1.   Durkin,  T.  H.,  Jaslovsky,  G.  S.,  and Boward,  W.  L.,  Operating
     Experiences with a Concentrated Double Alkali  Process,  American
     Power Conferences, April  23,  1980.

2.   Wagner,  N.  P.,  Adams,  L.  J.,  and  Ramirez,  A.  A.,  Technical  and
     Economic Factors for Evaluating Flue Gas  Desulfurization  Technologies,
     American Power  Conferences, April,  1978.
                                      496

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               STATUS REPORT ON THE WELLMAN-LORD/ALLIED
              CHEMICAL FLUE GAS DESULFURIZATION PLANT AT
               NORTHERN INDIANA PUBLIC SERVICE COMPANY'S
                       DEAN H. MITCHELL STATION
                              E. L. Mann
                Northern Indiana Public Service Company
                            Hammond, Indiana
                                  and
                              R. C. Adams
                               TRW Inc.
                Research Triangle Park, North Carolina
ABSTRACT
The Northern Indiana Public Service Company and the U. S. Environmental
Protection Agency entered into a cost-shared contract in June of 1972
for the design, construction, and operation of a regenerable flue gas
desulfurization (FGD) demonstration plant.  The system selected for the
project was a combination of the Wellman-Lord S0? Recovery Process and
the Allied Chemical S0? Reduction Process.  The FGD plant was to be
retrofitted to NIPSCO's 115 MW pulverized coal-fired Unit No. 11 at the
Dean H. Mitchell  Station in Gary, Indiana.  NIPSCO entered into contracts
with Davy Powergas, Inc., for the design and construction of the FGD
plant and with Allied Chemical Corporation for operation of the plant.
The FGD plant acceptance test was successfully completed on September
14, 1977.  The plant completed a two-year demonstration test period
during which information was collected and reported regarding pollution
control performance, secondary effects, economics, and reliability of
the system.  TRW, Inc. was the independent evaluator for the EPA through
October, 1979.  A follow-on EPA/NIPSCO contract of seven and one-half
months has recently been completed.  Operation of the plant continues.
                                    497

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PROCESS DESCRIPTION
Wellman-Lord S02 Recovery
The Wellman-Lord process consists of three major operating sections -
S02 absorption, purge treatment and S02 regeneration.
In the S02 absorption section,  residual fly ash in the flue gas is
removed by water scrubbing.   S02 is then, removed from the flue gas by
scrubbing with a solution of sodium sulfite.  The chemicals contained in
this solution remain completely dissolved throughout the absorber.  Flue
gas scrubbing with a clear solution, free from suspended solids, plugging
and scaling, is a fundamental  reason underlying the exceptional on-
stream reliability experienced  in the commercial operations of the
Wellman-Lord process.
The purge treatment section  selectively removes inactive oxidized sodium
compounds from a sidestream  of  the absorbing solution and converts this
material into a dry granular product which is marketed.
The third section of the Wellman-Lord process involves thermal regenera-
tion of the absorbing solution  to release the absorbed S02 as a concen-
trated gas stream and return of the reconstituted solution to the absorber.
The concentrated S02 gas may be converted to liquid S02, sulfuric acid
or elemental sulfur.  NIPSCO elected to use the Allied Chemical S02
Reduction Process to convert to elemental sulfur.

Allied Chemical S02 Reduction to Sulfur
Sulfur is recovered by Allied Chemical's S0? reduction process which
consists of two principal operating sections.
In the primary reduction section, more than one-half of the entering S02
is converted to elemental sulfur.  A key feature of this section is the
effective control of chemical  reactions between S02 and natural gas over
a catalyst developed by Allied  Chemical for this purpose.  Heat generated
by these chemical reactions  is  recovered and utilized to preheat the S0?
gas stream entering this section.
Packed bed regenerative heaters provide a rugged and efficient means for
achieving this heat exchanger function.  The process gas flow through
                                    498

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the regenerators is periodically reversed to alternately store and
remove heat from the packing; hence, the overall  section is thermally
self-sustaining.
Automatic control of the flow reversing cycles and other process con-
ditions achieves optimum performance in the system, with high sulfur
recovery efficiency and reductant utilization at all operating rates.
The gas leaving the primary reactor system is cooled in a sulfur condenser,
for condensation and recovery of sulfur product.   The remaining gas,
containing proper proportions of S02 and H2$ is processed through a
Claus conversion system for recovery of additional sulfur product.  The
Claus system off-gas is incinerated and recycled to the Wellman-Lord S02
absorber (see Figure 1).  Since startup in 1977,  5843 long tons of
sulfur have been produced.
PROCESS CHEMISTRY
The Wellman-Lord process is based on the chemistry of the sodium sulfite/
bisulfite system:  flue gas containing S0? is scrubbed with a sodium
sulfite solution which absorbs SCL, converting sodium sulfite to sodium
bisulfite:
     (a)  S02 + Na?S03 + H20   -*        2 NaHS03

The sodium bisulfite solution is regenerated by thermal decomposition.
Application of heat simply reverses equation (a):
     (b)  2 NaHS03
The SCL is recovered in a concentrated stream.
The concentrated stream of S02 gas is then reduced to high purity elemen-
tal sulfur in the Allied Chemical Process.  This conversion is carried
out in two steps.  In the first step, a portion of the SCL in the feed
gas. reacts with natural gas, yielding a mixture of elemental sulfur,
hydrogen sulfide, carbon dioxide and water vapor:
     (c)  2CH4 + 3S02   "»        S + 2H2S + 2C02 + 2H20
In the second step, H2S formed in the first step reacts with the remaining
S02 yielding additional elemental sulfur and water vapor:
                                    499

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                                                                                                    CM
                                                                                                    Secondjry
                                                                                                     Condenser
in
O
o
                                                          Figure 1.
                                   Wellman-Lord Recovery/Allied Chemical S02Reduction

                                               General Schematic  Flow Diagram

                                                NIPSCO Mitchell Unit No. 11

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     (d)  2H2S + S02   ±-—   3S + 2H20
The tail gas from the sulfur plant is incinerated and recycled to the
Wellman-Lord absorber.
TEST PROGRAM RESULTS
This section includes an analysis of the test results from the EPA
evaluation that was conducted by TRW.  The analysis focuses on the last
thirteen months of the two-year demonstration period.

Description of Test Program
The test program as originally designed consisted of three major test
phases:
     (1)  a baseline test
     (2)  acceptance testing
     (3)  a one year demonstration test and evaluation
                                                                        1  2
The initial baseline and acceptance tests have been described in detail.
The acceptance test was successfully completed in September of 1977 and
the scheduled one year of operation for demonstration testing followed
immediately.  During the demonstration year, operating experience was
limited due to both boiler and FGD related operating problems.  Operating
experience and operating problems were described at the FGD Symposium
held in March of 1979.   The test results have been reported.   These
test results were inadequate for fully evaluating the FGD process
because of those upsets caused by the boiler and thus external to the
FGD plant.  Modifications were begun during the latter half of the
demonstration year that prompted the decision to continue with a demon-
stration test program for another full year.  In this report, we will
focus on the operating and S02 removal performance of the Well man-
Lord/Allied Chemical FGD unit during the second year of demonstration.
The period covered is from October 1978 through October 1979.  It was
preceded by a second baseline test that provided up to date performance
and operating data on the boiler while the FGD plant was down and com-
pletely isolated from the boiler.
                                     501

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As we stated earlier, modifications were begun during the latter half of
the first year of demonstration.   Except for insulation of the inlet
ductwork, these modifications were completed during a scheduled boiler
shutdown in September 1978.   Our data show that the modifications ulti-
mately enhanced the performance of the FGD unit and of the boiler.   The
boiler was utilized during 93% of the second year of the demonstration.
With a dependable supply of flue gas to feed the FGD plant,  conditions
were quite favorable for gathering test data.   The modifications that
provided substantial improvement were as follows:
     (1)  Use of Captain coal.  Coal feeding problems were minimized
          when this coal was used.  Other corrective action  for improving
          coal feeding were to enlarge the coal  mill feed chutes and to
          increase capacity of the coal mills.
     (2)  Elimination of a boiler feedwater problem.
     (3)  NIPSCO agreed to remove a part of the heat transfer surfaces
          from the Ljungstrom air preheaters at some penalty in boiler
          efficiency.  With this modification, flue gas temperatures
          were maintained above the dew point and booster blower problems
          caused by wet operation were eliminated.
     (4)  Electrification of the FGD evaporator circulating  pump.
          Conversion from steam turbine to electrical drive  reduced the
          startup time.

The test program demonstrates performance of the Wellman-Lord/Allied
Chemical FGD process in these four major areas:
     (1)  Dependability of the FGD unit
     (2)  SOp removal performance
     (3)  Energy and raw material consumption
     (4)  Cost

The TRW test installation provided 10 or more measurements per hour of
flue gas composition, steam and electrical  energy consumption, and  the
boiler operating parameters  of interest.  One hour averages  computed
                                    502

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from these data served as the primary data base for most of the data
interpretations.  The amount of raw materials, natural  gas and soda ash,
and sulfur production were measured less frequently.

Summary of Results
The test program was designed to demonstrate guaranteed performance of
the Wellman-Lord/Allied process and its ability to meet these performance
criteria in a long term dependable manner and relative to the specific
flue gas conditions at the host site.  Since the FGD plant was designed
and sized for a specific load factor and specific flue gas characteris-
tics, the test also evaluated its operability over the normal range of
load variation and flue gas composition experienced during the second
demonstration year.  The results are summarized as follows:
     1.   Reliability of the FGD unit, hours operated/hours called upon
          to operate, was 61%.  The reliability record was established
          with virtually no redundancy built into the FGD unit.  Also,
          the evaporator was designed for only 80% of full boiler load.
          With limited surge capacity within the regeneration loop, the
          FGD plant was not able to operate to effect complete S02
          recovery during evaporator or reduction unit shutdowns.
     2.   The major sources of interruptions were
               the reduction unit
               the evaporator circulating pump
               the booster blower
               the evaporator
               startup time
     3.   Twenty four-hour average S02 removal efficiences of 85% to 92%
          were typical.  The pounds of S02 emitted  per million Btu of
          heat input varied from 0.25 to 0.94.
     4.   S02 removal was attained at boiler loads  in the  range of 53
          MWe to 85 MWe of the 115 MW boiler.  Some operation was achieved
          up to 93 MWe.  The lower limit was set by the  limiting turndown
          capability of the reduction unit.  The upper limit was set by
                                    503

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the capacity limitation of the evaporator as designed.  This
would not have been a limitation had the evaporator been
designed to match the full SOr, removal capability of the
absorber.  Since a substantial amount of energy largely as
boiler main steam was consumed by the FGD plant, the generating
potential of the boiler was actually about 95 MW at the FGD
maximum capacity limit of 85 MWe.
S02 removal was attained from flue gas with the following
characteristics relative to design:
•    SCL feed in excess of the expected plant capacity of about
     5400 Ib/hr was successfully treated for sustained periods
     of 24 hours and greater without loss of SOp removal  effi-
     ciency.  Overall for the second demonstration year,  S02
     feed averaged 4700 Ib/hr.
e    Flue gas flow rates were usually higher than the expected
     flow rate of 320,000 acfm by a substantial amount.  All
     flue gas flow rates in this report are at the design basis
     of 300°F and one atmosphere.
•    Inlet temperature, following modifications to the air
     preheater of the boiler to obtain higher temperatures,
     averaged 305°F.  Design basis temperature was 300°F.
The steam consumed by the FGD plant amounted to about 11% of
the boiler input energy.  Boiler derating averaged 9%.
Raw material consumption was as follows:
«    Soda ash average daily consumption was 9.9 tons.  Moles of
     sodium consumed averaged 10.6% of the moles of SOo removed
     from the flue gas.
•    Natural gas was consumed at a rate of 7.1 cubic feet per
     pound of sulfur produced.
The production of sulfur as a byproduct averaged 17-1 tons per
day of full operation.  The product was sold locally.
                          504

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FGD Dependability
There were various modes of operation depending on the availability of
equipment and on flue gas availability.  The principal operating modes
were as follows:
     Mode 1 -  boiler operating, FGD not operating.
     Mode 2 -  integrated operation of the absorber/evaporator and reduc-
               tion units without bypass of any of the flue gas.
     Mode 3 -  operation of absorber/evaporator with the flue gas bypass
               damper open.  Bypassing of the flue gas may or may not
               occur depending on the booster blower speed setting.
     Mode 4 -  operation of absorber/evaporator with the reduction unit
               not operating.  Recovered SCL (from evaporator overhead)
               is vented after dilution with flue gas from other units.

The FGD unit was considered to be fully operable only during Mode 2,
although that also may have been the case during some of the Mode 3
operation.  The exact operating status was difficult to determine while
the bypass damper was open.  However, failure to include any part of Mode
3 operation as fully operable time did not penalize the FGD process
unfairly because the amount of accumulated full operation time with the
bypass damper open was very low.  Mode 2 or full operation status does
not take into account the operation or performance of the purge treatment
unit.  The purge unit may or may not have been operating during Mode 2
operation and problems with the purge unit will be discussed later.
Figure 2 shows the reliability, hours of Mode 2 operation/hours called
upon to operate, for the thirteen months of the second demonstration
year.  Called upon hours are those boiler operating hours when  the
boiler is delivering flue gas and steam within the design range.   Figure
2 shows the FGD unit reliability factors plotted for each of the thirteen
months.  The overall average reliability was 61%.  The ups and  downs of
operating performance shown here may be summarized as follows:
     •    Best reliability was achieved during October and November,
          1978.  For a 57 day period, October 16 to December 11, inter-
          ruptions were minor and shortlived.  FGD reliabiltiy  was  99%
          during November.
                                     505

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CD
o
TOO


 90


 80


 70


 60


 50


 40


 30


 20


 10


  0
                   Oct
            Nov
 Dec

1978
Jan

1979
Feb    Mar    Apr    May   June    July   Aug    Sep
                                                       PERIOD
Oct
                                          Figure 2.   FGD Reliability Index

-------
     •    Operation was limited to 66% reliability during December to
          clean the evaporator heater and for reduction area repairs.
     •    The FGD plant went down on January 10 for 43 days to repack the
          evaporator circulating pump and to retube a sulfur condenser.
     •    Full operation was limited during late February and early March
          due to numerous mechanical problems and leaks.  The major
          problem during March was an outage of 16 days to overhaul  and
          realign the evaporator circulating pump.
     •    From April until October, FGD plant reliability averaged 73%.
          Recurring problems with the booster blower turbine speed
          control and with the reduction unit were the primary limitations
          to better reliability.
It should be noted that during the seven month period, April to October,
month by month reliabilities were fairly consistent, were primarily in a
range of 70-75%, and were 13% higher than the thirteen month average
reliability.
Table 1 identifies the equipment items that gave the most problems.   The
highest percentage of downtime was due to numerous interruptions of the
SOp reduction unit.  Since surge capacity for the scrubbing solution was
minimal, any interruption of reduction unit operation required that
either the evaporator be shutdown or recovered S02 be vented.  Usual
practice was to vent the SO^.
The major interruption of the reduction unit was a 35 day shutdown to
retube a sulfur condenser.  Without this interruption, the reduction
unit limited full operation during 7% rather than 17% of the called upon
hours.  The most frequent outages were those due to sulfur deposition,
leaks, and valve repairs.
With electric instead of steam turbine drive for the evaporator circu-
lating pump, emergency shutdown of the FGD plant was accomplished several
times without difficulty.  There were eight boiler shutdowns while the
FGD plant was at full  operation.  Four of the shutdowns were without
warning.  Two of the shutdowns were after a short warning period of less
than one hour.  The other two occurred with adequate advance notice and
the FGD shutdowns preceded the boiler shutdowns by 6 hours and 9 hours.
                                    507

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Table 1.  REASONS FOR INTERRUPTION TO OPERATIONS
en
0
CD






Equipment or
reasons
Reduction unit
Evaporator circulating pump
Booster blower
Startup and shutdown
Other equipments including absorber
Evaporator

Days of
interruption
59
28
18
17
10
8


% of called
upon time
17
8
5
5
3
2







-------
Startups were a different story.  Table 2 shows the startup time required
for the same eight boiler shutdowns.  Usual sequence after boiler startup
was to start the absorber/evaporator loop and flue gas flow first followed.
by the reduction unit after which the bypass damper was closed.   The
startup record of Table 2 indicates, perhaps, that more time is  required
for startup after the more lengthy shutdowns.  Otherwise, some of the
startups seem to be unnecessarily long.
The other reasons for FGD plant interruptions may be summarized  as
fol1ows:
     •    The evaporator circulating pump was down three times for
          repacking, for overhaul and for realignment of the motor
          shaft.  It was also down once to replace a seal attributable
          to interruption of the steam supply from the boiler.  Without
          steam, the condensate used for seal water was lost.
     •    The booster blower was down for relatively short periods but
          frequently.  Most of the problems centered around the  turbine
          governor and the gear reducer.  There were no problems associated
          with the internal surfaces of the fan itself.
     •    There was one interruption for cleaning the evaporator heater
          after it had plugged.
     •    The absorber operated essentially trouble free.  There was
          only one six hour interruption caused by an obstruction in the
          process water valve.
     t    Other problems accounted for less than 3% of the called upon
          time.  They include frequent replacement of the S02 superheater
          with an overhauled spare and repairs to the S02 compressor.
          These items of equipment are in the line feeding SO^ to the
          reduction unit.  Other interruptions were for instrument and
          duct leak repairs.

S0£ Removal
Removal efficiencies averaged 90% overall for the 13 months of operation.
These removal efficiencies were obtained during an accumulated 211 days
                                     509

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                                Table 2.    FGD PLANT STARTUP TIME

Boiler
down hrs .
3
3
34
100
3
138
11
3
FGD startup
time hrs
1
0.2
31
84
38
70
11
4
Startup
Absorber/evaporator
0
0
9
8
3
24
2
0
sequence, hrs.
Reduction
0.3
0.2
22
47
31
21
4
3

Bypass damper
0.7
0
0.2
29
4
25
5
1
295                  239                      46                      129                    65

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of Mode 2 operation of the FGD unit.  Thirty day average removal  efficien-
cies varied only from 88% to 93%.  The range of values increases  as
averaging times decrease.  Figures 3 and 4 are frequency distributions
of 24-hour averages and one-hour averages, respectively.  These data
show that S02 removal performance compared to design (90%) and to the
operating control point of 89% was as follows:
                                             	% of time	
           S02 Removal                       24-hr Avg.     1-hr  Avg.
          90% and greater                       60            52
          89% and greater                       84            78
          85% and greater                       97            97
It is seen that removal efficiencies of less than 85% occurred infre-
quently.
One-hour averages were accumulated to determine removal performance at
the longer averaging times.  Figure 4 shows that S02 removal was  less
than the limit of 89% for 22% of the time.  The plant operated at removal
rates of 85% or better for 97% of the time.  The absorber was operated
to achieve about 89% or higher removal rather than 90% removal.  This
was because operating control for S02 removal was set to reduce the S02
concentration on a diluted basis by 90%.  Since dilution amounted to
about ten percent, primarily as moisture, the actual removal was  about
one percent less than the reduction in concentration.  The S02 removal
data presented in this report have been corrected for dilution.
The flue gas being treated had the following characteristics.  The
characteristics of primary interest are:  S02 feed, flue gas flow rate.
and temperature.
     S00 Feed.   Sulfur level in the as received coal averaged 3.09 wt%.
       ~t
Confidence limits for this mean value at the 95% level were 2.99 wt% to
3.19 wt%.  A coal of 3.16 wt% sulfur was used for design of the FGD
plant.  The estimated range, based on a distribution of two standard
deviations from the mean, was 2.6 wt% to 3.6 wt%.
                                     511

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   100
    90
    80
    70
    60
 <£.
 Q
VI

UJ
to
ce
UJ
a.
     50
    40
     30
     20
    10
         70
                              .    •    I    il
80
88  90
                                                                             100
                                  S02REMOVAL,  %
    Figure 3 .   Cumulative Frequency Distribution of 24-Hour Average S02 Removal


                                         512

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   100
   90
   80
   70
u   60
Q
Ld


£   50



VI

u
10


2   40
UJ
U
o:
LJ
0.
   30
   20
   TO
       70
Figure 4.
                               .mil
                         80                 88  90



                               S02REMOVAL, %
100
                  Cumulative  Frequency Distribution of One Hour Average SCLRemoval



                                        513

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Concentration of S02 was expected to be 2185 ppmv,  wet basis,  at a coal
sulfur level  of 3.16 wt%.   The equivalent S02 feed  rate for this concen-
tration is 4842 Ib/hr at the design flue gas flow rate of 320,000 acfm
and the design equivalent boiler load factor of 80%.   Actual  flue gas
flows were somewhat higher due to higher than expected excess  air caused
by excessive  inleakage believed to be at the air preheaters.   The absorber
was designed  to receive a volume of flue gas equivalent to 100% load
factor and to remove the corresponding amount of S02  at inlet  concen-
trations of at least 2185 ppmv.  While the capacity to handle  flue gas
flow rates and S02 feed rates equivalent to 100% load factor was demon-
strated for short periods, sustained operation was  only possible at load
factors slightly better than 80% because of the limited capacity of the
evaporator and limited surge capacity in the regeneration loop.  This
limited the capacity of the boiler during high demand that was in addition
to the derating effect from FGD plant steam consumption.   While perform-
ance at high  load was not fully demonstrable, minimum sustainable operat-
ing rates were demonstrated during turndown tests.   Full  operation at  53
MW was sustained for four days.  Table 3 summarizes the inlet  conditions
of this test.
               Table 3.   FGD PLANT MINIMUM'SUSTAINABLE
                          LOAD TEST RESULTS

     Length of test                               4 days
     Average  load                                53 MWe
     Flue gas flow                              237,000 acfm
     S02 feed                                     3,381 Ib/hr
     S02 feed                                     2,069 ppmv wet
     Oxygen in flue gas                             7.5 vol. % dry

Below this operating level, the FGD plant is limited  by the turndown
capability of the reduction unit.  The absorber/evaporator was operated
down to 44 MWe.  It must be remembered, however, that these minimum
loads are generator output after derating due to the  steam requirements
                                    514

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of the FGD plant.  Equivalent loads relative to flue gas flow and boiler
heat input are 50 MW generating potential at the 44 MWe level  and 60 MW
generating potential at the 53 MWe level.
     Boiler Load.   The FGD plant operated'with S02 removal  rates of 89%
or better at 24-hour average loads from 53.MWe to 93 MWe.   However,  85
MWe was usually the upper limit for operation.  Figure 5 presents the
load factors for each 30-day period of the second demonstration year
during Mode 2 operation of the FGD plant.  The FGD plant was expected to
operate at a boiler load potential of 92 MW and did indeed meet or
exceed this capacity during three of the 30-day periods.  For the rest
of the time, the boiler was demand limited and the load factors remained
below the 92 MW level.
     Flue Gas Flow Rate.   While boiler load was generally below the
design level, the reverse was the case for flue gas flows.  This was due
to higher than expected excess air in the flue gas.  Figure 6 shows  flue
gas flow rates as a function of both the actual generator output and the
boiler load potential.  Flue gas flows of 320,000 acfm, the design
level, were attained at 71 MW of generator output or 80 MW of load
potential.  At a FGD load limit of 85 MW, the flue gas flow rate was
over 360,000 acfm.  At the load potential of 92 MW, the design point,
the flue gas flow rate was nearly 360,000 acfm.  Since the absorber was
designed for full load, the greater volume of flue gas presented no
apparent problems for the booster fan or the absorber.
     Excess Air.   The high flue gas flow rates are explained by the
higher than expected amount of excess air that can be attributed primarily
to inleakage air believed to be entering at the air preheaters.  Oxygen
levels in the flue gas averaged 8.0% by volume compared to an expected
qxygen level of 5.6%.  On average, the additional amount of air would
increase the total quantity of flue gas by about 17%.  At higher than
average loads, the excess air averaged a little less than the overall
average and would add a little less than 17% to the quantity of flue
gas.
     Temperature^   Inlet temperatures averaged 305°F during the second
demonstration year.  However, 38% of the hourly average temperatures
                                    515

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o
«r
o
to
       120
       100
        80
        60
        40
        20
                                Generated Load


                                Load Potential
                                                                             FGD Expected Capacity
                                                                                           I      1
                                         XJ
                                          flJ

                                         4J
            Oct    Nov    Dec    Jan     Feb

                         1978    1979
Mar    Apr    May    June   July    Aug    Sep.    Oct



   PERIOD
                           Figure n    Boiler Load and Load Loss During FGD Operation

-------
*/>

g

LU
r>

U-
100
                                    Actual  Load
      400
                   	Load  Potential
 <0
o

O
O
 o
 re

o
o
o
      300
200
         50
                           60
70
80
90
                                                    GROSS LOAD, MW
                              6.   Flue  Gas  Flow Rates at Actual Load and Load Potential

-------
were below 300°F but virtually all  of these temperatures were above
280°F.  It should be noted that these are single point temperatures well
within the flue gas stream and do not reflect temperatures at and near
the duct surfaces.  There were, nevertheless, no problems attributable
to wet flue gas.

Energy Consumption
A significant amount of the steam produced by the boiler was consumed by
the FGD plant, primarily for operation of the evaporator for recovering
the S02 and regenerating the scrubber solution.   Boiler main steam from
the superheater at 1800 psi and 1000°F was let down and desuperheated to
obtain steam for the FGD plant at 550 psig and 750°F.   This steam was
used in steam turbines to drive the booster blower, S0? compressor and
the evaporator circulating pump.   However, before the  start of the
second demonstration year, the evaporator circulating  pump drive was
electrified to eliminate the startup and shutdown problems that occurred
when high pressure steam was interrupted by unscheduled boiler shutdowns.
The turbine exhaust steam along with additional  550 psig steam that had
been let down through a pressure reducing valve was desuperheated further
and used for process heat, primarily at the evaporator.
Actual steam consumption (at 550 psig, 750°F) varied from 52,000 Ib/hr
to 59,000 Ib/hr during the second demonstration year.   In Btu's, this
was equivalent to 11% of the boiler input energy derived from fuel and
derated the 115 MW boiler by 8% at the average boiler  load of 77 MWe.
In addition to steam consumption, about 700 kW of electricity was con-
sumed, exclusive of the evaporator circulating pump motor.  This increases
the total energy requirement to about 12% of the boiler heat input
derived from fuel.  This derated the boiler another 0.6%.  The total
derating is equivalent to an electric production loss  of 10 MW of gener-
ator output.  Power to the evaporator circulating pump was not metered
but is estimated at 330 kW,

Raw Material Consumption
Soda ash is used as makeup sodium carbonate for the scrubbing process.
Usage is determined by buildup of inactive constituents in the absorber/
                                    518

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evaporator loop, such as sulfate and thiosulfate, that have to be purged.
Any loss from the system due to leaks would also require soda ash makeup.
High soda ash consumption during the first demonstration year were due
to leaks at the bottom collector tray of the absorber that were repaired
before start of the second demonstration year.  These leaks effectively
aborted the estimation of purge rates during the first year.
For the thirteen months of the second demonstration year, 2273 tons of
soda ash were consumed, for an average daily consumption of 9.4 tons per
day, using the total operating days of the absorber/evaporator as the
time base.  The performance guarantee for acceptance was 6.6 tons per
day at the design levels of flue gas flow and inlet S02.
Natural gas is used as the reductant for converting the SCL to elemental
sulfur.  It is also the fuel used to incinerate the tail gas emitted
from the reduction process.  The tail gas is returned to the inlet of
the absorber after incineration.  It was necessary that the incinerator
continue to be operated during shutdowns for destruction of the reduced
sulfur forms that desorb from the reduction unit refractory materials.
Thus, there is a corresponding improvement in unit consumption of natural
gas with improvement in reliability.  Table 4 shows that slightly over 7
cubic feet of natural gas was consumed per pound of sulfur produced.
            Table 4.  NATURAL GAS CONSUMPTION

      Annual consumption, million cf               54.1
      For process use, %                           87.9
      For incineration use, %                      12.1
      Average consumption during
         mode 2 operation, cf/hr                   9745
      For process use, %                           92.5
      For incinerator use, %                        7.5
      Process gas/sulfur produced,
         cf/lb                                      6.2
                            (continued)
                                    519

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                        Table 4 (continued)
      Total gas/sulfur produced,
         cf/lb                                      7.1
      Consumption during shutdown,
         % of total                                  5.6
This meets the design expectations.  Average consumption was 9745 cf/hr.
of which 7.5% was consumed by the incinerator.  In contrast, the inciner-
ator consumed over 12% of the total gas overall for the second demonstra-
tion year and is a consequence of the 61% FGD plant reliability factor.

Purge Treatment Limitations
The purge unit as initially designed was to have treated a small purge
stream removed from the regeneration loop, to effect a separation of
sodium sulfate from most of the sulfite/bisulfite components, and to dry
the sodium sulfate to produce a salable product.  The "wet" end of this
purge treatment system performed satisfactorily but the dryer had a
capacity of only about 50% of that needed.  The requirements on the
purge unit and the drying problem will  be discussed in turn.
The amount of purge to be treated is a  function of the formation of
sulfate and possibly thiosulfate during absorption.  Attempts were made
by TRW to determine the amount of sulfate formation during absorption
but these efforts were frustrated by inability to obtain correct flow
measurements and uncertainties about the specific water balance across
the absorber.  However, the data seem to indicate that sulfate formation
is a function of oxygen concentration in the flue gas.  Since excess air
levels were higher than design expectations, higher than design purge
rates might be necessary.  Purge rates  were not measured directly.
However, an average purge rate for the  period April through October has
been estimated at between 10.6  and  12.4%.   Purge rate  is  the ratio  of
moles sodium in purge to moles SOp removed from flue gas, expressed as a
percentage.  The estimate was determined from soda ash consumption and
the calculated amount of SO,, removed.  A purge rate of about 10% was the
                                    520

-------
value indicated during the design phase of the project.  In the aggregate,
the above information seems to point to actual purge rates higher than
design, the magnitude of which is unclear.  As stated before, the process
up to drying seemed to perform satisfactorily.
Dryer tests performed by Davy McKee determined that the dryer would not
work, even at design rates.  There had always been a question of whether
the sulfate dryer actually had heat duty design capacity.  In May of
1979, tests verified that the dryer did not have design capacity.  The
purpose of the test was to demonstrate the heat capacity of the dryer
with a water feed onto a sodium sulfate bed in the dryer.  If the maximum
rate could be reached with water, the dryer was then to be tested with
the sodium sulfate solution recovered from the purge solution.
The maximum dryer capacity achieved during the test was approximately
.66% of the design heat duty.  Capacities of 59-66% of design were main-
tained for 2-1/2 days.  However, after operating for 2-1/2 days at 59-
66%, the motor tripped out several times because of an amperage overload.
When the motor tripped out, a buildup of solids was observed at the
discharge end of the dryer.  To prevent overloading the motor, the water
feed rate was reduced, so during the last 2-1/2 days of the test, the
dryer capacity dropped to 45-50% of design.  At this point, further
testing was abandoned.
Possible solutions include:
     1.   A more concentrated feed fed to same dryer.
     2.   A dryer of different design.
     3.   Addition of an antioxidant to the absorbing solution.
Replacement of the equipment capable of attaining design capacity would
cost approximately $500,000.  Alternates to the equipment replacement
were sought.  Antioxidants to reduce sulfate formation were considered.
Tests of EDTA (Ethylene Diamine Tetra Acetic Acid) were run April - May of
1980.  The tests were terminated after five days of an intended  two-week
test because of unrelated equipment failure.  The too brief test period
indicated a possible 50% reduction in sulfate formation.  Additional
testing of EDTA is planned.
                                     521

-------
                    OPERATING AND MAINTENANCE COSTS

                     NIPSCO UNIT NO.  11  FGD PLANT

Operating, Maintenance and Improvement Costs are listed from the

period of January 1, 1979, through April  30, 1980.

Operation and Maintenance - Offsites  Facilities                  $ 154,160
     (including booster blower, flue  gas  ductwork
      and dampers, utilities system)

Operation and Maintenance - FGD Process                            6,061,205
     (includes by-products storage and loading,
      raw materials unloading and storage,  and
      Allied Management Fee)

Total FGD Costs before By-Product Credit                           6,215,365

Credit for By-Products                                              104,963

Total FGD Operation/Maintenance Costs after                      $6,110,402
     By-Product Credit

No amortization costs are included above.
                                    522

-------
    COAL DATA AND UTILITIES - January 1, 1979, through April,  1980
High Sulfur Coal Burned, Tons                          349,121
Average BTU/#                                           10,586
Average Sulfur %                                             2.85
Steam Used, Pounds                                 455,000,000
Boiler Feedwater Used,  Pounds                       29,128,000
Condensate Returned to  Gen. Sta., Pounds           333,120,000
Condensate Dumped, Pounds                          151,008,000
Electric Power, Kwh (Including 500 HP                6,472,000
     Circ. Pump Motor)
Natural Gas,  Ft3                                    57,642,000
Service Water,  1000 Gallons                          2,784,000
Elemental Sulfur Sold,  Long Tons                         2,668
Sulfate Sold, net  tons  (no dry sulfate  was                 139.6
     produced in 1980)
                                     523

-------
         NORTHERN INDIANA PUBLIC SERVICE COMPANY
              DEAN H.  MITCHELL STATION
          UNIT NO. 11  S02 DEMONSTRATION PLANT
              OPERATING HOURS GRAPH
1.   Solid line indicates Unit No.  11 or S02 Plant is in opera-
    tion.

2.   Definition of Unit No.  11 being in operation is:  Unit
    synchronized on line regardless of megawatt load.

3.   Definition of S02 Plant being in operation is:

    a.   Receiving all of flue gas from Unit No. 11.
    b.   No S02 bypassed to the Unit 6-11 stack.

4.   Unit 11 operating conditions required for S02 Plant Operation
    are:

    a.   Unit 11 operating on high sulfur coal at 46 GMWE (min.).
    b.   Sufficient main steam available (530 PSIG minimum).
    c.   Sufficient demineralized make-up water available.
    d.   Unit 11 supplied utilities available (electricity,
        boiler feed water).
                            524

-------
OPERATING HOURS
mi — 	 _
,^— .*•. 	 • Bijj 	 ..-...- 	 , ,,,.
^iH
1
1
1
1
I6;30 AM **"* Repair evapor
I pump. Repair
| tank agitator
I 1st sulfur co
sulfur con den





















ator circulating
dump dissolve
Tube leak in
ndenser. Retube
ser.















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~~~~||
1
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                        Unit No. 11
                                                      71
                                                      12
                                                      13
                                                      14
                                                      15
                                                      17
                                                      119  i
                                                      22
                                                       2.3
                                                       28
                                                       29
                                                       30
            525

-------
                      OPERATING HOURS
Plant
 Retube sulfur condenser.
 Absorber & evaporator
 start-up.  Expansion
 joint leaks in S02
 reduction area.
Unit No. 11
                                                                           9

                                                                          no
                                                                          11
                                                                           12
                             13
                             14
                                                                           15
                                                                           16
                                                                           17
                                                                           18
                                                                           19
                                                                           20
iAIJ° ™- BH V
___2; 10 PM 	 	 £laus expansipn, joint leak.
12:20 PM
-aT/tf-W.."**" S0o superheater repair.
Replace evaporator circ.
pump packing due to loss of1
seal water caused by boiler
Trin & lac|c o_j? emers. steam.
Nozzle steam leak in S02
• — . 	 	 5-e.duct:laa, ja^^-




_
m
ii
6:31 PM Vacuum pump trip. 1
7.42 PM ™iSiffl
ffil^S^
fe »f»i

p^1 1
p^'-fc'.^( 1 .
us



22 ;
23
2i
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26
27
28


!
	 i
                                  526

-------
                          OPERATING HOURS
S02 Plant
Unit No. 11
I
ll
1

1
1


1
1

1

.
.
.


.
_


S(>2 superheater
&
1:55 AM 	
£-.30 PM1™ Glaus convertei
joint repair.

L2:28 PM|g||
s
H
m
P^epair evapora
pump shaft .
i









\
Booster Fan Tr

: repair.
r expansion

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tor circulating










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15
16
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      Clean tail gas  piping.
                                                                              25
                                                                              !26
                                                                              30
                                                                               :
                                     527

-------
OPERATING HOURS
?C? Plant
HI
ii
7:55 AM""" S02 superheater leak.
JH:30 AKJpSl

||
]||
[itJl Plugged tail gas line.
tiff
||
ii
H
„ iiral

H
fU
83

il
3:15 ?Mp|!i| Incinerator Trip - Condensa-
^J^CLJ'SLs!'*''35' tion pj3 burner Controls .
H*'1'''?'
US
|j|| Bypass louver dampers tripped
^•*m open on loss of control air.
H
~|i
m
Louver dampers tripped open -
K',f, High duct pressure.
9:00 AM ^^ Evaporator heat exchanger
tube pluggage.
High vibration on evap . circ.
piimn mqt-pr.



Unit No. 11
US
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6
7
8
9
10
11
12
13
14
15
16
17
(
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„ . _..!

20 !
21
*". <*»
' 2.L
"•>'•
^
25
26
27
28
£ y
30

           528

-------
                           OPERATING HOURS
S02 Plant
Unit N'o. 11
P Continue Rvap. CIrc. Pump
|_ . 	 EleC. MoJinr^Pjopp I r


_^_ ^
V
ISO. Plant Start-Up

12:10 PM |H
IS
II
H

ir niRB t\fciuctxon r> mituoWn J.TI
11:45 AM ^^ Preparation for boiler outage


:J:15 PM Repair SOo Superheater
: K
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1 ^:r>-'
1 .,..., f
fl
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«->:43 AM r...
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4
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6
7
8
9
10
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12
13
14
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17
18
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                                                                                      vO
                                                                                      -J
                                                                 "suTator TaTTTirr ^~~~\

                                                                            not   '
                                      11.55 P"M     close.

-------
OPERATING HOURS
S02 Plant Unit No. 11


j

i







SO Plant in Start-Fp Mode
11:15 AM F^
JJ
H
H
Hi
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m
Brief Main Steam Supplv
Interruption
8 '
il
fat"!
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&
H:l5 $>f fete Plugged Makeup Water Valve
12:30 PM S-v"
£•/??,
• 5:00 AM P^'S Reduction Unit dovm duo to
j i-&Sfl low inlet S02 to FGD Plant
| Pepair leaks in inlet flue
P.TK duct.
SO Plant in start-up mode.

6:10 PM
8 : A 5 AM Repair Expansion Joint.
bi
12:AO PM |j^

P-eheat Stop Valve Repair



4:14 AMH




1

9
I


r^vyt^s!!
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11
fes
P"^"^
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|
Bl Failure of 11-F. F.T). Fan
H Motor

Si
IP
1
*•
i Trial ^-'un on mixture1 01
I Hir,h and Medium Sulfur Goal.
1 Unsatisfactory
\ let S07 to FGT1
due to low In-
Plant.
B
II
if
s

IPS

2
3
4
5
6
1
8
9
10
11
1 0
13
1A
15
i
16 i
17
	 1
To
19
20
21 ;
'2: :
i
13
2A !
25
26
M I27
Si
p
iff

1
28
.29
30

           530

-------
                                 OPEEAT1NG  HOURS
      SO, Plant
            Inspect  booster fan speed
            reducer
             Inspect booEffer fan speed
             reducer
            Repack main steam pressure
            reducing valve . Testing and
            inspection of reduction unit
            mixed gas systen.      	
11:25 AM
Reduction uni~t dovm~fo
conduct turndovm tests.

Pluggago in mixed pas
cooler and sulfur condenser.
                                           Unit No. 11
                                                  -fp-
                                                  —!i
                                                                        10
                                                                                     11
                                                                                     13
                                                                                     14
                                                                         15
                                                                         16
                                                                                     20
                                                                                      23
                                                                                      25
                                                                                      26
                                                                                     i">,
                                                                                      28

1 Los
t Northeast fUts.
29
in'
                                            531

-------
OPERATING HOURS
SOj
1:20 PM r Plant in
Start-up' mode.

1:40 PM
1
8:00 AH m.
S

« Change R02 Superheater.
L___fe

•T
'
•

1



i
033
I
i
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i
-i
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•i
9:51 PM iii East Unit Aux.
4 KV
Breaker failure. Cold re-
heat line water hammer on
start-up. Repair and inspec
tion of cold reheat line.



1:5P Pit T
i
1:
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1


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^
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1
2
3
4
^
6
7
8
" S
10 S.
!
11
12
13
, J
14
15
16
17
18
19
21
•C i-
'.|23 |
i

5:24 AM*8"" Precipitator Repair,
1 ] : 50 PM
P
K
P
•2*1
2> i
26
27
26
i
29
4:57 PM iiLb Hi^h ^en^rator voltape. j-5 ;
'i:26'AM trip - rhebftCat fallnrCT"
31
            532

-------
                          OPERATING HOURS
SO2 Plant
     TAIL GAS INCINERATOR
     MALFUNCTION
     BROKEN GOVERNOR LINKAGE
     ON BOOSTER FAN
     BOOSTER FAN TRIPS -
     SPililD INDICATOR ERR01
     CAUSED OVERSPEED TRIP
     LEAK IN BOOSTER FAN
     TURBINE GOVERNOR STEAM
                                      5:00  am
                                      7:51  am
Unit No. 11
  130 KV YARD FAULT
                                                                               11
                                                                               12
                                                                               13
                                                                               14
                                                                                --J
                                                                               16
                                                                               i7
                                                                               18
                              21 :
                                                                                22
                                                                                23  1
                              124  ;

:1
t1
••£
i
1
4

27
28
29
!_
                                                                                O "^
                                                                                oO
                                      533

-------
                                 OPERATING HOURS
       SO.-,  Plant
                                           Unit No. 11
                                                                                      - • — \
                                                                                      4 ,
                                                                                      5

                                                                                      6
5:20 pmHll  BROKEN BOOSTER FAN
     F mm  TURBINE GOVERNOR VALVE
                                                                        10
5:30 pm
             STEM
                                                                                      11
                                                                                      12
9:15 am
BOOSTER FAN SPEED
REDUCER MALFUNCTION
                                                                                      13
                                                                                      14
                                                                                      15
                                                                                      16
                                                                                      17
                                                                                      •'2G
                                                                                      J22  ;

                                                                                       23
                               11:27
UNIT 11 TURBINE
BLADE FAILURES
                                                               -ML
                                                                                       !25
                                                                                       26
                                                                                       27
                                                                                       29
                                                                                       30
                                              534

-------
                          OPERATING HOURS
SO, Plant
                                                 Unit No.  11
    CONTINUED SCHEDULED
CONTINUED OUTAGE FOR
                               1 i
    OUTAGE WlTH UNlT 11"
TURBINE BLADE REPAIR AND
SCHEDULED TURBINE AND
                                               BOILER MAINTENANCE
                                                                              5
                                                                             ac
                                                                              12  !
                                                                              13

                                                                              14
                                                                              15
                                                                              17

                                                                              18 I
                                                                              19 i
                                                                                 1
                                                                              20
                                                                              22
                                                                               24
                                                                               25
                                                                               26
                                                                               27

                                                                               28

                                                                               29

                                                                               30
                                      535

-------
OPERATING HOURS
S02 Plant
'
CONTINUED SCHEDULED
OUTAGE WITH UNIT 11.




























L__
Unit No. 11
CONTINUED SCHEDULED
OUTAGE FOR BOILER AND
TURBINE MAINTENANCE.





















12:10 PM — - UNIT START-UP
l P • 1 7 PM
2:53 PM 3:21 PM
9 : 11 PM ~ 9:53 PM
8:15 PM
11:30 PMw
8: 35 PMp,™, /:
12:13 AM
HIGH EXHAUST H001) .
6:^5 PM,^ TEMP. & VIBRATION.
12:32 AM BUM 5.50 m
12:50 AM TRIP CHECKS.
12 : 40 AM *•* k : 30 AM

1
2
*
4
5 }
6
7
8
9
10
11
12
13
14
15
16
17
18
.!•">
J20
21
22
23
J2/,
I
2^
2b
27
23
• 29
3')
:, 31











8
8
?
T''
JL
UD







1


i



1

i
            536

-------
                          OPERATING HOURS
S02 Plant
Unit No. 11


















.bUUbThK J?'AW STAftl'-'UP MD
BALANCING.
FGD PLANT START-UP IN
PROGRESS .


BOOSTER FAN BALANCING
COMPLETE .
CONTAMINATED CONDENSATE
RETURN. SHORTAGE OF
BOILER FEEDWATER.

CONTAMlWA'm; UUWUKWbATK
RETURN .
t

BOOSTER FAN SHUT DOWN
TO ALLOW REPAIR OF
ORIFICE CONTACTOR.
1 BOOSTER FAN START-UP.
If
-- 	 if
ss
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fe
.1:30 AM ^

1 : 30 AM D
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8:19 PM «
1:28 AM I
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:




8: 11 "AM"
11:27 AM






1
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1
a
1^s PRECIPITATOR REPAIR.

sis
mat -•" -
1

ii
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m
if
~ hti
S»
^B
if
2H
•lufej
^:-:l
ial CONTROL VALVE MALFUNCTION.
?"'Poi
?;*f'
i*^'";
MS,^
*„,-•#'>".}
^''•""-'7l'Lf .,..„.,._ ...„,„„ 	 	 	 	 	 ...„,„,*, „ ,ui 	 	
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'y:-^";fe ,

gft-l'S
COLLECTOR RING BRUSH HOLDER
B SHIFTED - LOST EXCITATION.
1
P
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1
ill
i :^$
*-..fts
^-.V':^
S:V. 4
»toa
^


3
4i
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• 1
7 1
8 '
9
LO
11
12
13 !
14 1
5
15 H
^
16 c
17
,, i
19 ;
20
i
21
22
•
23
24
25
26 i
27
28
29
I
30
31
                                      537

-------
NORTHERN INDIANA PUBLIC SERVICE COMPANY
        FGD PLANT OPERATING HOURS

DATE
l
2
3
4
5
6
7
8
9
10
11
12
13
14
15
16
17
18
19
20
21
22
23
24
25
26
27
28
29


FEBRUARY
FGD PLANT
Orifice
Contactor
Repairs




On Tl:28am
Off l:45pm *•"
Piping Leak In
Reduction Area
On l:45pm g^gg
Off 10: 25am Leak In Shell Of "A"
..^JK.egenerator
8 : 00am
S02 Plant Available
But Condensate Quality
Problem in Generating
Station

On. 2 : 03pm
Off 4:I5pm a""™1
Leak In Regenerator
On 9; 48am
Off 8:IZam «»""Leak~~tn Regenerator
On 10:29am plffl
B
s
OFF 10" tiOain"™ Replace Leaking SO? S.
On 2: 00pm *
B
S am #11 To Come Off Line




, 1980
UNIT NO, 11
in
H
||
H
|p
Off 3: 42pm H|Turbine Control Valve
On 4: 45pm ^^Malfunction
B
n
I
il
H
,
n
H
S
1
1
B
s
	 fe
H
if
m
IP
Htr* H
H
Off 10: 40pm ^Kenerator H2 Leak





DATE
X
2
3
4
5
6
7
6
9
10
11
12
13
14
15
16
17
18
T) J
20
21
22
23 |
, , , — .
2, ]
25 |
26
27
2e
29 J
' j
- •: 1
                       538

-------
NORTHERN INDIANA PUBLIC SERVICE COMPANY
        FGD PLANT OPERATING HOURS

DAIh
i
2
3
4
5
6
7
8
9
10
11
12
13
14
15
16
17
18
19
20
21
22
23
24
25
26
27
28
29
30
"31

MARCH
FGD PLANT
SO/, Compressor
Problems


]

.
1
	 s
i


On 0:10pm ,,,,„„ 1
Off 2: 20pm S02 Leak In Reduction
~ , 	 Area Piping
On 0:45pm mi&
iff j
11
H
Off 4: 22pm KB Incinerator Control
Failure
On 10: 20am ___.
Off 12:01pm^™Unit 11 Scheduled To
Be Off











On 1 1 : 45am mmm
Off 3: 50pm *"HH" Sulfur Blockage In
Reduction Area
, 1980
UNIT NO, 11
H
11
B
n
S
H
m
11
ill

— — II
H
iS
gi
H
«li
-|;«
I'M
~~A| »^;.;;'' " " ~"
Off 7?09pmifiiM Remove Turbine Stop
Valve Screens And
Check H2 Seals




On 1 • 02pm j^p'fgi
Off 10:56pmHlFalse Trip - Ground
s-fj,™ Protect ion Relay
On 6: 22am fe^f
|||

|||
irt


DATE
1
2
3 \
4 i
5 !
6 \
7
8
9 1
10 :
11 j
12
13
14
15
r~nn
•*. 1* *
i? i
18 |
H
19 |
_£fH
~2l!
22 ",
23- -;
24
25
26
27 .
I __»
i w :
29 !
30 !
31
	 a

                        539

-------
              NORTHERN INDIANA  PUBLIC  SERVICE  COMPANY
                       FGD PLANT OPERATING HOURS
                                   APRIL, 1980
DATE,
  1
FGD PLANT
    Sulfur Blockage
                     In Reduction Area
      On ll:AOam
      Off l:40pm
          UNIT  NO, 11
                   DATE
                                                            .'2
    Sulfur Blockage
                     In "B" Claus  Reactor
  10
  11
                                                            10
                                                            11
  12
  13
  14
  15
  16
  17
  18
  19
      On 10:15am
                                                            12
                                                            13
                                                            14
                                                            15
                                                            16
                                                            17
                                                             IS
                                                             19  i
  20
  21
  22
  23
  24
      Off IrAOpm
    Unit 11 Off
Off 3:48pm
Condenser Leaks
                                                             20
                                                             21
                                                             2-3
                                                             24
                                         On 9:56am
                                                             25
  26
  27
  28
    S02 Plant
    Start Up
      On 11:20am
                                    26
                                    27
                                                             28
  29
  30
                                                            •29
                                                            •30
                                         540

-------
               NORTHERN INDIANA PUBLIC SERVICE COMPANY
                        FGD PLANT OPERATING HOURS
                                     MAY, 1980
DATE
                FGD  PLANT
                     Repair
                     Bearing
           UNIT NO.  II
DATE
                     Failure
                     In The
                     Evaporator
                                                        'alse Trip - Genera-
                                                        or Protection Relay
  10
                     Pump Motor
      l:15pm
                       Plant  Available
      1:25pm
                  .But No Steam From Unit
 11
                                                                              10
  11
  12
                   S02 Plant
                     Start Up
                                      11
                                                                              12
  13
  14
  15
    On 10:30am
    Off l;45pm
                     Reduction Area S09
                   Leak & SC>2  Compressor
                   Turbine Governor
                                      13
                                      14
                                      15
  16
  17
                   Steam Leak
                   SC>2 Plant
pff 2:32am
                                                         Dispatcher  - Low
                                      16
  17'
  18
                   Available
               System Load
  19
                   S02 Plant  Start Up
                                          On 9:28am
      Dn l:05pm
                                                                              20
                                                                              21
      Dff  7:00pm
                                                                                22
                                                                                23
                                                                                24
                    SC>2 Plant Available
                                                                               25
  26
                    Low System Load
                                         )ff 2:27am
               Dispatcher - Low
 '26
  27
                                                       System Load
                                           Zh 9:27am
                                           Off A;29ptn
                                       27
28
                                                        recipitator Problem
                                       28
  29
                                         1:40pm
              "Available
  30
                                                       Dispatcher - Low
  31
                                                       System Load
                                        541

-------
REFERENCES
1.   R.  C. Adams, T.  E.  Eggleston, J.  L.  Haslbeck, R.  C.  Jordon, and
     Ellen Pulaski.  Demonstration of WeiIman-Lord/Allied Chemical
     FGD Technology:   Boiler Operating Characteristics,  EPA Contract
     No. 68-02-0235 (1977).
2.   R.  C. Adams, S.  J.  Lutz, and S.  W.  Mulligan.   Demonstration of
     Wellman-Lord/Allied Chemical FGD Technology:   Acceptance Test
     Results, EPA Contract No.  68-02-1877 (1979).
3.   F.  A. Ayer.  Proceedings:   Symposium on Flue  Gas  Desulfurization
     Las Vegas, Nevada,  EPA Contract No.  68-02-2612 (1979).
4.   R.  C. Adams, J.  Cotter, and S. W. Mulligan.   Demonstration of
     Wellman-Lord/Allied Chemical FGD Technology:   Demonstration Test
     First Year Results, EPA Contract No.  68-02-1877 (1979).
                                     542

-------
          MAGNESIUM FGD AT TVA:  PILOT AND FULL-SCALE DESIGNS
                                  by

                             E. G. Marcus
             Chemical Engineer  - Gaseous Emission Control
                      Tennessee Valley Authority
                     Chattanooga, Tennessee  37401
                             T. L. Wright
          Mechanical Engineer  - Mechanical Engineering Branch
                      Tennessee Valley Authority
                      Knoxville, Tennessee  37902
                              W. L. Wells
              Program Manager - Gaseous Emission Control
                      Tennessee Valley Authority
                     Chattanooga, Tennessee  37401
                               ABSTRACT
     This paper discusses pilot and full-scale magnesium flue gas desulfurization
(FGD) designs by TVA.

     The full-scale (600-MW equivalent) magnesium FGD design is for operation at
high and low load factors for a high sulfur coal.  After a process and system
chemistry (magnesium sulfite/bisulfite) description, the paper describes the FGD
equipment and system operation which includes an onsite acid plant.  The second
part of the paper discusses information on a test program and schedule of a pilot
plant being considered by TVA to verify the magnesium FGD design.
                                        543

-------
               MAGNESIUM FGD AT TVA:  FULL-SCALE DESIGN
INTRODUCTION

     TVA's involvement with magnesium flue gas desulfurization (FGD) systems
has included some testing of MgO on the 1-MW cocurrent scrubber pilot plant at
Colbert Steam Plant in 1976, a 10-MW cocurrent prototype system at Shawnee Steam
Plant in 1978, and various economic studies.1'2'3'4  The use of lime or lime-
stone FGD systems requires large land areas for disposal of the calcium sludge
produced.  A regenerable FGD system eliminates the calcium sludge, provides a
salable byproduct, and regenerates the absorbent for S02 removal.   United Engi-
neers and Constructors (UE&C) assisted TVA in the process design of the FGD
system and provided detailed engineering support, especially in the magnesium
regeneration area.


PROCESS DESCRIPTION/SYSTEM CHEMISTRY

     The magnesium FGD design uses magnesium sulfite-bisulfite chemistry for
S02 absorption, operating at a pH of approximately 6.0.   After absorption of
S02 by magnesium sulfite to form magnesium bisulfite, magnesium oxide is added
to the absorber recycle tank to react with the bisulfite and precipitate mag-
nesium sulfite.  The sulfite can exist as tri- or hexa-hydrate depending on
startup and operating conditions.  The equipment is being sized to operate with
either compound.  In the trihydrate mode, the magnesium salts (10  percent solids)
will be dewatered to 70 percent solids and then dried to remove all free water
and most of the bound moisture (see Figure 1).  The use of a sulfite storage
silo provides the ability to operate the absorption and dewatering areas com-
pletely independent of the downstream regeneration area and acid plant.  The
calciner is designed to decompose the magnesium sulfite (with an average of
1/2 mole of bound water per mole of magnesium sulfite) and sulfate (with 7
mole of bound water per mole of magnesium sulfate) into magnesium  oxide and
S02.  At a calciner operating temperatures of 1800°F, only 60 percent of the
sulfate is decomposed.  In actual operation the thermal decomposition of sul-
fate would be optimized to give the highest necessary percentage decomposition
at the lowest temperature.  The offgas from the calciner is designed for an
S02 concentration of 17 volume percent for feed to a single contact acid plant
Since the acid plant tail gas goes back to the main plenum, the S02 emissions
from the acid plant are part of the overall plant S02 emissions.

     Both the Philadelphia Electric Company's (PECo) experience at Eddystone
and the brief TVA experience at Shawnee indicates that there is little, if any,
solid magnesium sulfate formed as a solid in the absorber recirculating material.
The dissolved magnesium sulfate level in the absorbing slurry would be about
30 percent (by weight) using only the liquor in the trihydrate centrifuge cake
to the dryer as a purge stream.  However, this 30 percent is based on 10 percent
oxidation of the absorbed S02 to sulfate, 60 percent decomposition of sulfate
                                        544

-------
en
-P*
01
                                                                                                                                     	 UOUirV'SLURRY

                                                                                                                                     	SOLID

                                                                                                                                        GAS

                                                                                                                                     (S) SPARE
                                                              Figure  i: FGD   System   Process   Flow  Diogram

-------
in the calciner, and a trihydrate mode of operation (70 percent solids in the
centrifuge cake).   The PECo experience shows less than 10 percent oxidation
but at a higher operating pH in the absorber.   Operation at the lower pH may
produce more oxidation and a hexahydrate crystal reducing the amount of liquor'
evaporated in the rotary dryer.  The hexahydrate cake is easier to dewater thafl
the trihydrate.  This operation would raise the dissolved sulfate level in the
slurry to well-in-excess of 30 percent by weight.

     In order to provide flexibility of operation and for thermal protection
of the baghouse used for final magnesium particulate collection before the
acid plant, a spray dryer was placed between the calciner and the equipment
used for final magnesium particulate removal.  The spray dryer will use cen-
tra te from the centrifuge containing dissolved magnesium sulfite, bisulfite,
and sulfate.  In this manner, magnesium value in the form of MgSOs and MgSC>4
can be recovered.   This sulfite/sulfate mixture will be recycled to the sul-
fite silo for feed to the calciner.  Since there is a 60 percent sulfate
decomposition in the calciner, this use of the spray dryer allows for control
of the dissolved sulfate in the absorbing slurry, depending on actual operating
conditions.  For the design case, the sulfate level will be 24 percent MgS04
(by weight).


FGD SYSTEM EQUIPMENT

     In the absorption area, particulate, chlorides, and SOz are removed by
four (4) venturi-type prewash and absorber modules.  The venturi with its own
two-stage mist eliminator removes chlorides, 863, and fly ash in a separate
liquor loop.  Any chlorides which are not removed in the venturi loop will
form magnesium chloride in the absorber loop and could cause corrosion problems
in the regeneration area and acid plant feed gas clean-up system.  The blowdown
from the venturi recycle tank is neutralized in a separate facility with hydrated
lime and is then pumped to the plant disposal area.  The venturi liquor loop is
not neutralized and, therefore, operates at a pH of less than one.  In addition
to the S03 and chlorides removed in the venturi, additional dilute sulfuric
waste acid from the acid plant feed gas humidification/cooling towers and wet
ESP's are added to the venturi recycle tank.  This acid blowdown from the acid
plant feed gas clean-up system results from the water quenching of the calciner
offgas which contains about 0.6 volume percent 80s.

     To raise the venturi liquor pH to about 1.0, consideration is being given
in the design to pumping the acid plant blowdown directly to the neutralization
facility or to the absorber recycle liquor tank.  In theory, the waste acid
stream would form more magnesium bisulfite in the recycled liquor and require
more magnesium oxide in the absorber recycle tanks.  This would increase the
load on the regeneration area and acid plant but increase the amount of sul-
furic acid recovered and decrease the lime required for neutralization.  Of
the anticipated lime requirement for neutralization, 50 percent is required
for the acid plant feed gas clean-up system blowdown.  In either case, the low
pH and high chloride concentration will require corrosion protection of the
                                        546

-------
equipment.  For the venturi-type prescrubber, besides Inconel 625 for high
abrasion areas and FRP internals, the mist eliminators could be factory-
installed on special Inconel strips to avoid field installation of the blades.
An organic lining could be used to protect the carbon steel venturi shell.
Efforts would have to be made to ensure that there is minimal interior work
after lining installation (such as factory-installed mist eliminator blades).

     The S02 absorbers and their two-stage mist eliminators are designed for
operation in a cocurrent gas and slurry mode at 4.6 meters per second (15 fee:
per second) and an L/G of 4.5 liters per actual cubic meter (34 gallons/1000
acf)j and for mist elimination with horizontal gas flows of 6.1 meters per
second (20 feet per second).  The cocurrent absorbers are based on TVA's ear-
lier test .work with cocurrent absorbers at Colbert (1 MW) and Shawnee (10 MW).
Gas/slurry flows in the absorber/mist eliminator, especially the wet elbow
(180° turn) where the bulk of the entrained slurry is removed (see Figure 2),
can cause large variations in the gas velocity profile and produce solids
deposition on the mist eliminator.  The absorbers could be 316L stainless
steel; a need for higher grades of alloys is not anticipated due to the low
concentration of chlorides projected for the absorber slurry.

     There is no reheater in this design since saturated flue gas can be mixed
with linscrubbed flue gas after the scrubber for the flue gas reheat.  The scrub-
ber .fans have Inconel 625 rotors and 316L housings and the bypass fans, if needed,
would be Corten construction.  The lining for this very corrosive flue gas would
require extensive corrosion resistance due to the mixture of water vapor (scrub-
bed gas) and SOs/chlorides (bypassed gas), below the average boiler flue gas
acid dew point.

     The absorber recycle pumps and tanks are designed for normal slurry serv-
ice, similar to a limestone FGD system except for the use of a waterless seal
to assist in water balance maintenance.  Since the liquor in the centrifuge
cake (going to the dryer for evaporation) is only 35 GPM and any seal water
for these large 10,000 GPM recycle pumps would be at least 10 to 15 GPM per
pump (for a total of 60-90 GPM for the six (6) operating pumps), the use of
seal water for the slurry would require a purge of magnesium liquor to main-
tain the absorber loop water balance.  With all evaporation of water for
quenching the flue gas taking place in the venturi portion of the process, the
major water loss from the absorber-regeneration section is through the centri-
fuge cake into the drying system.  Since each GPM lost to blowdown to allow
for water in-leakage from the pump seals was worth $200,000 in makeup magensia
value over the life of the plant, TVA designed for pumps that did not require
seal water.  These types of pumps had been used successfully at Philadelphia
Electric Company (PECo) to help maintain a water balance.

     The regeneration area required several difficult decisions.  Since the
calciner offgas is at 1800°F, economic considerations dictated some heat be
recovered.  Based on PECo's experience, the original design of a shell and
tube heat exchanger to preheat fludizing air would present major operating
difficultues caused by the fouling of tube side heat transfer surfaces.  The
                                         547

-------
Figure  2.  Cocurrent  downflow  absorber  "wet elbow"  design
                            548

-------
  th^h  Off8as contains traces  of  S03  and  the  latter  apparently recombines
TVA H    re8enerated magnesium oxide  to form  a  solid sulfate.   Although the
IVA aesign has MgO product recovery cyclones  which are more  efficient than
those at i^Co  there is some  indication  that  the  recombination is  S03 control-
lea, or a aitrusion limited reaction.  Therefore,  no  matter how efficient the
product recovery cyclones, there will  always  be recombination and  potential
subsequent pluggage.  The method chosen  to  avoid  this problem in the design  is
to preheat the magnesium sulfite solids  being fed to  the  calciner  in a manner
which can be called "suspension heating."   The sulfite solids at ambient tem-
perature from the silo are injected  into the  1800°F calciner off gas  after the
recovery cyclones.  The sulfite solids are  preheated  and  then recovered in the
sulfite cylones.  Although the inlets  of these high efficiency cyclones are
small, very little pluggage would  be expected due to  the  high gas  velocities
ia the cyclones.  This type of solids  preheating  is now used in the  cement
industry and its successful operation  in magnesium FGD requires that sulfite
 solids not be heated to the decomposition temperature during suspension heating.

     The other difficult problem in  the  regeneration  area concerned  the use  of
 either an electrostatic precipitator (ESP)  or a fabric filter for  final mag-
 nesium oxide particulate removal before  the off gas passed to the acid plant.
 Any of this particulate which reaches  the acid plant  is lost from  the regen-
 eration loop and may poison the acid plant  catalyst if not removed by the
 humidification or gas cooling towers of  the acid plant feed gas clean-up sys-
 tem.  The TVA design required 99 percent removal  of the particulate  remaining
 after the three sets of upstream cyclones.   Originally for the design concept
 it was desirable for the final MgO particulate collection device to  operate  at
 temperatures in excess of 600°F, collect greater  than 98  percent of  the MgO
 and provide reliable operation.  At  first an ESP  was  selected over a fabric
 filter.  The fabric filter's  maximum operation is about 500°F; therefore, it
 is not suitable for this application.  However, this  selection was before the
 addition of a spray dryer for sulfate  control to  the regeneration area and
 before investigations were carried out on ESP collection of magnesium oxide.
  The change from an ESP to a fabric filter was finally resolved based on the
  operating characteristics of  ESP collection of magnesium oxide and the reali-
  zation that once the spray dryer was added, there was no reason to worry  about
  high temperature excursions (greater than 500°F)  affecting  fabric material.
  PECo operated a pilot ESP on  the regeneration offgas and verified the  informa-
  tion that had been accumulating from ESP manufacturers and  magnesium  oxide  sup-
  pliers.  Effective ESP operation on  magnesium oxide  requires  temperatures in
  excess of 600°F and would be  preferable  at  700°F.  In other systems  this  may
  have been acceptable but the  proper  operation of the spray  dryers requires  the
  largest temperature differential possible for maximum flexibility in control-
  ling sulfate concentrations.  A fabric filter would  allow  operation at the
  original design temperature of 450°F for final particulate  removal.
                                         549

-------
FGD SYSTEM OPERATION

     The magnesium FGD system design has an onsite acid plant containing two
trains and with a total capacity of 350 tons per day.  There are four 750,000-
gallon storage tanks which can provide up to 60 days of storage.  The acid plant
can produce either 93 or 98 percent acid, depending on market conditions.  The
key to the system operation is the fact that storage silos for magnesium oxide
and magnesium sulfite allow decoupled operation of the regeneration area/acid
plant from that of the power plant.  The absorber and dewatering/dryer areas
are sized to treat the required flue gas at full load.  Although the future
yearly capacity factor for this FGD system would be significantly less than 60
percent, these systems must be sized to accommodate full load operation during
peak periods.

     The regeneration area and acid plant are not designed to follow load as
are the absorbers (three operating and one spare), the centrifuges (four), and
the rotary dryers (two).  The regeneration area is gas flow dependent and the
acid plant is 862 dependent.  Therefore, a sulfite storage silo will be located
after the rotary dryer.  Correspondingly, there is a magnesium oxide storage
silo for the regenerated magnesium after the recovery cyclones.  Since the sea-
sonal electric loads will probably not correspond with the seasonal industrial
acid demand, typical operation will probably be as follows:  high load on the
absorbers (filling the sulfite silo) with low load on the regeneration/ acid
plant (drawing down the oxide silo); or low absorber load (drawing down the
sulfite silo) with high load on the regeneration/acid plant (filling the oxide
silo).

     The second section of this paper provides information on a test program
and schedule of a pilot plant being considered by TVA.  The research and devel-
opment areas of concern are identified for each of the major process steps.  A
number of research and development tasks which would provide the base technology
for the successful operation of the full-scale magnesia FGD system are discussed.
                                        550

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                 MAGNESIUM FGD AT TVA:  PILOT DESIGN


INTRODUCTION

     As mentioned earlier, land availability around existing and future fossil
fuel steam plants could limit the disposal of wastes for any FGD system that
has a "throwaway" product.  However, it is generally agreed that magnesium FGD
technology is not as well developed, particularly insofar as the regeneration
portion of the process is concerned, as that of lime/limestone scrubbing.


PILOT OBJECTIVES

     The operation of the pilot plant will simulate the full-scale TVA magne-
sium FGD design in every practical way for the purposes of this study.  Pri-
mary objectives of the pilot plant program are as follows:

     1.   Develop valuable in-house experience with the MgO process.

     2.   Anticipate potential problems with the TVA MgO process chemistry or
          equipment.

     3.   Evaluate the long-term effects of process contaminants such as fly
          ash, chlorides, and trace elements which evolve from the burning of
          coal by reliability runs of several months' duration.

     4.   Study the formation and properties of magnesium sulfite hexahydrate
          versus trihydrate crystals with respect to potential solids handling
          problems.

     5.   Study the regenerated MgO absorption capability after several cycles.

     Secondary objectives are to develop process design improvements and innova-
tions such as sulfur production, and the use of coal for drying and calcining
through additional studies not yet completely defined.  All these studies will
be done in conjunction with EPA.  The secondary objectives will be met in such
a way as not to impact the schedule for fulfillment of primary objectives.
Most of these objectives are process related and have general application to
magnesium FGD technology.

     TVA has retained the magnesium FGD design architect/engineer, United Engi-
neers and Constructors, Inc., and had the magnesium FGD design scaled down to
the 1-MW level.  The pilot plant would not include the acid production facilities.

     Sections of the pilot plant (primarily the regeneration and drying sec-
tions) will be "skid" mounted to provide maximum flexibility in operation.
Skid mounting will allow the operation of the pilot plant to be broken down
into a Phase I and Phase II operational scheme.  Phase I operation will be
                                        551

-------
chiefly concerned with the primary objectives of the pilot plant as previously
listed.  Phase II operation will be concerned with additional studies.

     These additional studies will develop process design improvements and inno-
vative concepts.  Examples of such improvements and innovative concepts may
include but not be limited to the following:

     1.   Using coal instead of oil in the drying and calcining of the
          magnesium sulfite.

     2.   Spray drying for SC-2 absorption instead of wet scrubbing.

     3.   Testing of a sulfur-producing technology using coal as a reductant
          instead of natural gas or oil.

     The current schedule calls for the pilot plant to start up in the fall of
1981, with the intention of providing operational experience and some solutions
to the problems mentioned earlier.


RESEARCH AND DEVELOPMENT AREAS OF CONCERN

     Identified in the following subsections for each of the major processing
steps are more details of a number of research and development tasks (outlined
above) which would provide base technology for the successful operation of a
full-scale magnesium FGD system.


PRESCRUBBER

     The pH of the prescrubber solution has been calculated to be lower than
1.0 due to dissolved HC1 and H2S04-  In the particulate scrubber, the hot flue
gas is contacted with a slurry of fly ash and river water.  Most of the particu-
late (fly ash) and hydrogen chloride, and a variable fraction of the sulfur
trioxide, are removed in the scrubber liquor.  The blowdown slurry from the
particulate scrubber, therefore, is acidic and the water may contain high con-
centrations of dissolved solids, trace metals, toxic organics, and radionuclifle;
either leached out from the fly ash or absorbed from the flue gas.

     In this acidic environment only expensive alloys such as Inconel 626 or
Hastelloy G, or an organic lined metal alloy, may be suitable.  Should the
prescrubber be made of materials such as 316L stainless steel, addition of a
neutralizing agent such as caustic soda or lime/limestone would be necessary
to raise the pH to at least 3.0.  This addition would be undesirable since it
introduces additional dissolved solids into the system and may complicate the
disposal of the prescrubber blowdown as described later.  Various materials of
construction (through the use of coupons) will be tested in the pilot plant
venturi-type prescrubber to identify those alloys and organic lined metals able
to withstand the low pH environment without neutralization to a higher pH.
                                        552

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S02 ABSORPTION

     For this portion of the FGD process there remain two concerns:  (1) the
chemical effects of chlorides, fly ash, and dissolved magnesium salts on sul-
fite oxidation and (2) magnesium sulfite trihydrate (MgS03»3H20) vs. hexahy-
drate (MgS03'6H20) formation.  Experience has shown that the trihydrate
crystals can be obtained during steady-state operation, but during startup,
shutdown, or during nonsteady-state operation hexahydrate crystals have been
observed.  The crystals of the two hydrates have widely different handling
properties and this fact can introduce difficulties in the solids separation
and drying steps of the process.  The operating parameters affecting the above
items will be investigated.

     As an alternative to wet scrubbing TVA is considering spray drying and
subsequent fabric filter collection for S02 absorption as part of the Phase II
operational scheme.  Although definite plans have not been formulated, a spray
dry/fabric filter would be investigated to determine optimum operating condi-
tions.  The regeneration section from the Phase I tests would be used to decom-
pose the MgS03 to MgO and S02.  This FGD system would have the advantages over
the wet scrubbing system of no flue gas reheat and elimination of the drying
step.


DRYING

     Two control schemes described below will be investigated to determine
optimum operating parameters with regards to (1) sulfite to sulfate oxidation
during drying, (2) MgS03 decomposition, and (3) economical operating conditions.

     With the first scheme, two variables—the airflow (primary combustion air
and dilution air) and fuel flow—will be controlled in series to maintain a
constant dryer gas discharge temperature.  Fuel flow control follows combustion
chamber temperature, thereby increasing lag time for response and decreasing
control accuracy.  The dryer discharge gas temperature control point senses
the gas temperature and demands an inverse gas flow change before a fuel adjust-
ment has fully responded to its initial demand.  Also, the refractory lined
combustion chamber is an excellent heat sump which further increases lag time
for fuel adjustment.

     For the second control scheme, common practice in other industries is to
maintain constant gas flow at a maximum rate that has an acceptable dew point
and carry-over dust load; the discharge gas temperature then controls the fuel
flow directly.  Such a control method will eliminate one of the two control
variables and may reduce control lag time to a minimum.
                                         553

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REGENERATION

     There are two concerns about the fate and possible accumulation of minor
elements such as calcium, sodium, and chlorine in the regeneration portion of
the FGD process:  (1) Does the chlorine leave the process perhaps as HC1, or
does it remain in the process tying up magnesium salts, and (2) Does a molten
liquid phase of MgCl2, NaCl, or CaCl2 exist in the calciner offgas?

     A predicted composition of the calciner feed stream for the magnesium FGD
design is summarized in Table I.5  At the desired operating temperature (1800°F)
the output from the calciner was thermodynamically calculated and is shown in
Table 2.6  Thermodynamically, at 1800°F the decomposition of MgS04 to MgO, S03,
S02> and 02 is favorable; calcium is present in the solid phase as CaS04, and
a liquid sodium sulfate/chloride melt is predicted.  Most of the chlorine in
the calciner feed leaves the system in the gas phase as HC1.


                    TABLE 1.  CAICINER SOLIDS FEED


          Compounds                          Weight Percent
MgS03
MgS04
MgCl2
Na2S04
CaCl2
Ash
70.0
8.9
9.8
0.2
0.4
10.6
                                   Total          99.9
     Experience with PECo's prototype calciner (actually an entrained-bed reactor
rather than a traditional fluid-bed reactor) at its Essex Chemical test facility
has revealed that approximately 30 percent of the MgSOs feed forms hard, che&ji--
caily unreactive MgO pellets.  These pellets do not discharge with the MgO fines
overhead in the offgas but rather eventually fill the calciner bed and have to
be ground before reuse in S02 sorption.  Examination of the high density MgO
pellets indicates a possible double salt, Mgs Ca(S04)4, as the root cause of
pellet formation.7  The MgO fines generated overhead are very fine (3-30
microns) and difficult to handle, thereby causing transportation and storage
problems.

     As discussed earlier, in the full-scale design fouling of the she11-and-
tube air preheater exchanger by MgS04 was also experienced at PECo's regenera-
tion test facility at Essex Chemical. ,The plugging was rapid and rendered the
                                        554

-------
heat exchanger unusable.  The magnesium sulfate is thought to form in the  cal-
ciner offgas by recombination of MgO and the relatively small amounts of highly
reactive 803.  The recombination should be avoided not only because of heat
exchanger plugging, but also because it introduces a recirculating load of MgS04
in the system that is inactive for S02 sorption.

     The regeneration study will determine whether the predicted sodium sulfate/
chloride melt and CaS04 in the gas phase are the cause of the problems at  Essex
Chemical and, if so, will determine the most economical solution to the shell
and tube preheater fouling.  Specifically, we propose to examine, as a function
of the operating parameters (1) MgS03 and MgS04 decomposition, (2) MgO pellet
formation, (3) MgS04 recombination, (4) optimum product yield, and (5) chlorine
composition and purge rate.


          TABLE 2.  OUTLET CALCINER GAS COMPOSITION AT 1800°F


                                                  Mole Percent

        Gases

          C02                                          9.4
          H20                                          5.5
          N2                                          53.7   ,
          NO                                       8.75 X 10"-3
          HC1                                          3.4   „
          Cl"                                      1.40 X 10
          C12                                      2.11 X 10
          S02                                         11.6
          S03                                          0.3   o
          MgCl2                                    1.60 X 10"J
          02                                           1.7


        Liquids

          Na2S04                                   1.16 X 10"^
          MgCl2                                    1-26 X 10 \
          NaCl                                     3.75 X lO""3
        Solids

          MgO                                         13.6
          MgS04
          CaS04                                        0.7
                                                     100.0
                                        555

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DESIGN IMPROVEMENTS AND INNOVATIVE CONCEPTS

     In addition to spray drying and subsequent fabric filter collection for
S02 collection, TVA is considering the following:  (1) the use of coal or a
coal-oil mixture in place of oil in the drying and calcining of the magnesium
sulfite and (2) the direct production of elemental sulfur from the decomposi-
tion of MgS03.  Although no definite plans have been formulated, minor modifi-
cations to the Phase I drying and regeneration equipment is all that is
necessary to test the coal-fired option (excepting, of course, the addition of
coal handling facilities).  For the production of elemental sulfur, TVA has
obtained the services of P. S. Lowell to expand upon an earlier EPA study on
this topic.8


SUMMARY

     Thus, we have identified proposed research and development studies on a
number of potential problems.  These problems, it is felt, are soluble with
current state-of-the-art engineering knowledge.  The magnesium FGD design
offers promise as a technically viable, economically feasible process for
recovering SOa as a useful product—sulfuric acid.
                                        556

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REFERENCES
1.   Robards, R. F.; Cole, R. M.; Morasky, T. M.; "TVA's Cocurrent Scrubber
     Evaluation," Winter Annual Meeting of the Air Pollution Control Division
     of ASME, Atlanta, Georgia,  1977, 77-WA/APC-8.

2.   Robards, R. F.; Moore, N. D.; Kelso, T. M.; and Cole, R. M.;  "Cocurrent
     Scrubber Evaluation:  TVA's Colbert Lime-Limestone Wet Scrubbing Pilot
     Plant," EPRI FP-941, Research Project 537-1; January 1979.

3.   Marcus, E. G., and Wells, W. L., "Magnesium Oxide Testing on the iO-MW
     Cocurrent Scrubber at the Shawnee Steam Plant," in press.

4.   McGlamery, G. G.; Torstrick, R. L.; Simpson, J. P.; and Phillips, Jr.,
     J. F.; Conceptual Design and Cost Study; Sulfur Oxide Removal from Power
     Plant Stack Gas, EPA-R2-73-244, May 1973.

5.   Lowell, P. S., "Technical Memorandum 009-02-02, Equilibrium Program and
     Thermodynamic Data Base for TVA Reducing Calciner," May 1980.

6.   Lowell, P. S., "Technical Memorandum 009-02-08, Thermodynamic Analysis of
     the TVA MgS03 Colbert Pilot Calciner," May 1980.

7-   Kelmer, A. D., "Magnesia Flue Gas Desulfurization—Status of Development
     and Needed Technological Support, Letter from Charles D. Scott (Assoicate
     Director, Chemical Technology Division, ORNL) to J. Frederick Weinhold
     (Director, Division of Energy Demonstrations and Technology,  TVA),
     February 21,  1980.

8.   Lowell, P. S.; Corbett, W. E.; Brown, G. D.; and Wilde, K. A.; Feasibility
     of Producing Elemental Sulfur from Magnesium Sulfite, EPA-600/7-76-030,
     October 1976.
ACKNOWLEDGEMENTS

     The authors wish to thank and acknowledge the assistance of the following
persons without whose help this paper could not have been written and assembled:
B. A. Anz and C. C. Thompson, Jr., of United Engineers and Constructors.  We
also wish to acknowledge the financial assistance of the Environmental Protection
Agency in the pilot plant program.

     The contents of this paper do not necessarily reflect the views and policies
of the Tennessee Valley Authority or the Environmental Protection Agency, nor
does mention of any trade names, commercial products, or companies constitute
endorsement or recommendation for use.  This is a government publication and
not subject to copyright.
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