EPA-65Q/2-74-Q22

   March  1974
Environmental Protection  Technology  Series

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                               EPA-650/2-74-022
     COKE  CHARGING
 POLLUTION  CONTROL
     DEMONSTRATION
               by

            J. H.  Stoltz

   Jones and Laughlin Steel Corporation
         Pittsburgh, Pa. 15219
       Contract No . CPA 70-162
         ROAP No. 21AFF-03
      Program Element No. 1AB013
  EPA Project Officer: Robert V . Hendriks

      Control Systems Laboratory
  National Environmental Research Center
Research Triangle Park, North Carolina 27711

           Prepared for

  AMERICAN IRON AND STEEL INSTITUTE
        150 EAST 42nd STREET
       NEW YORK, N. Y. 10017

              and

 OFFICE OF RESEARCH AND DEVELOPMENT
U.S. ENVIRONMENTAL PROTECTION AGENCY
      WASHINGTON, D. C. 20460

            March 1974

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This report has been reviewed by the Environmental Protection Age
and approved for publication.  Approval does not signify that
contents necessarily reflect the views and policies of the Agency,
nor does mention of trade names or commercial products consti u
endorsement or recommendation for use.
                                  11

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                             ABSTRACT

    This report presents the results of demonstrating a coke oven
charging system designed to reduce emissions sufficiently to meet
future air pollution control requirements and improve the
environment on top of the battery for operating personnel.  The
work included detailed engineering,  construction, and testing of
a prototype system on an existing battery with a single gas
collecting main.

    The results of the demonstration show that although a signi-
ficant reduction in emissions has been attained, it will be
necessary to modify the system with a double gas off-take to
approach smokeless charging conditions.  This system can be
applied to new batteries or to existing batteries where a double
gas off-take exists or can be obtained by some means such as a
second collecting main or "jumper" pipes.

    The battery top environment was improved for the larry car
operator as a result of performing the charging sequence from
within an air conditioned cab.  Although a lidman is required
on the top side of the battery, his work conditions have been
improved as a result of performing lidding and dampering opera-
tions with the larry car.

    This report was submitted in fulfillment of Contract CPA
70-162 under the joint sponsorship of the Environmental
Protection Agency and the American Iron and Steel Institute.
Work was completed in March, 1974.
                              111

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                            CONTENTS
                                                             PAGE
Abstract                                                     iii

List of Figures                                              vi
List of Tables                                               ix
Acknowledgments                                              x
SECTIONS

I        Conclusions                                          1
II       Recommendations                                     11
III      Introduction                                        15
IV       The AISI/EPA Charging System                        20
V        Charging Equipment Description                      30
VI       Project Results - Smokeless Charging                66
VII      Project Results - Process Control                   86
VIII     Project Results-- Performance of Equipment          96
IX       Application of System to New Batteries             167
X        Application of System to Existing Batteries        176
XI       Cost Data                                          180
XII      Bibliography                                       190

XIII     Glossary                                           192

XIV      Conversion Factors                                 194

                               iv

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                            CONTENTS





SECTIONS





XV       Appendices                                         195




         A.  Oven Pressure Measurements




         B.  Reliability Data                                198




         C.  Leveler Bar Investigation                      213




         D.  Emission Data                                  250




         E.  Empty Oven Tests                                272




         F.  Battery Dimensional Variations                  280




         G.  Ascension  Pipe Particulate  Sampling            284
                                v

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                               FIGURES

 NO.                                                        PAGE

 1        Charging Emissions - AISI/EPA Car                   2
 2        Charging Emissions - Conventional Car               3
 3        Emissions - Conventional Charging                  16
 4        Emissions - Conventional Charging                  17
 5        Charging System - Single Gas Off-Take              21
 6        AISI/EPA Charging System Automation                22
 7        AISI/EPA Larry Car                                 31
 8        Cross-Section    P-4 Battery                       32
 9        Coal Charging Car Arrangement                      33
10        Coal Charging Car Arrangement                      34
11        Drop Sleeve Feeder Operation                       35
12        Automatic Lid Lifter                               37
13        Place Oven On-The-Main                             39
14        Oven Dampered-Off                                  40
15        Ascension Pipe Cleaner                             42
16        Operation of Positioning System                    44
17        Positioning System Arrangement                     45
18        Lid Lifter and Drop Sleeve Hydraulic Panel         47
19        Environmental Unit Arrangement                     49
20        Environmental Unit - Top View                      50
21        Pusher- Charging Car Interlock                     53
22        Carrier Current Signal System                      54a
23        Leveler Door Operator                              57
24        Leveler Door                                       58
25        Existing P-4 Ascension Pipe                        60
26        New Design Ascension Pipe                          61
27        Self Cleaning Steam Nozzle                         63
28        Charging Hole Lid                                  64
29        Butterfly Oscillation Angle                        74
30        Coal Level Profile During Charging                 77
31        Jumper Pipe Charging                               80
32        Jumper Pipe Arrangement                            81
33        Gravity Feed Hopper Test Arrangement               97
34        Drop Sleeve Seating                                99
35        Hopper Fatigue Crack                              101
36        Coal Level Sensor                                 110
37        Bent Steam Linkage Rod                            118
                                VI

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                              FIGURES

                             (continued)

                                                            PAGE
NO.                                                         -

                                                            120
38        Ascension Pipe Operating Linkage
39        Ascension Pipe Operating Linkage
40        Broken Standpipe Cap Hinge Lugs
41        Damper Stop Mechanism
42        Self Aligning Gooseneck Cleaner                   127
43        Gooseneck Cleaner Operation Description           128
44        Positioning System Accuracy Data                  131
45        Insulation of Proximity Switch                    13 9
46        Open Web Leveler Bar                              1^7
47        Leveler Bar Bulb Angle Cross-Section              150
48        Solid Web Leveler Bar                             151
49        Wedge-Shaped Leveler Bar                          152
50        Empty Oven Tests                                  157
51        Ascension Pipe Ejector Performance                159
52        Double-Piston Self-Cleaning Steam Nozzle          163
53        Ascension Pipe Elbow Covers                       164
54        Oven Pressure Recording                           197
55        Definition of Larry Car Availability              201
56        Definition of Larry Car Production Index          205
57        Larry Cars on P-4 Battery                         206
58        Larry Car Performance Record                      207
59        Larry Car Performance - Data Form                 208
60        Larry Car Performance - 3 Months                  208a
61        Microstructure - Leveler Bar Steel                221
62        Leveler Bar Web                                   222
63        Leveler Bar Temperature Distribution              224
64        Leveler Bar Temperature Distribution              226
65        Leveler Bar in Coke Oven                          227
66        Leveler Bar Thermocouple Locations                228
67        Thermocouple Switching Circuit                    230
68        Leveler Bar Temperature                           235
69        Leveler Bar Temperature                           236
70        Leveler Bar Temperature                           237
71        Leveler Bar Temperature                           238
72        Leveler Bar Temperature                           240
                                VII

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                              FIGURES

                           (continued)

NO.                                                         PAGE

73        Leveler Bar Temperature Rise                      241
74        Leveler Bar Heating Time                          243
75        Orifice Flow Meter                                273
76        P-4 Battery Dimensional Growth                    281
77        Photomicrographs of Suspended Solids in Tar       286a
78        Ascension Pipe Coal Carry-over Sampling           292
79        Coal Sampling Apparatus                           293
                               Vlll

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                             TABLES

NO.                                                        PAGE

 1       Charging Emissions - Single Gas Off-Take            4
 2       Charging Emissions - Jumper Pipe                    6
 3       Larry Car Charging Emissions                       67
 4       Larry Car Charging Emission Data                   69
 5       Charging Emissions, Variable Steam Pressure        71
 6       Tar Samples P-4 Battery                            90a
 7       Production Tar Analysis                            91
 8       Coke Oven Gas Analysis                             93
 9       Gum Content of Circulating Wash Oil                94
10       Larry Car Capital Costs                           181
11       Pusher Machine Capital Costs                      182
12       Battery Modification Capital Costs                183
13       Charging System Options                           184
14       Leveler Bar Costs                                 185
15       Larry Car Maintenance Requirements                187
16       Other Charging Maintenance Requirements           188
17       Type of Larry Car Failures - December             209
18       Type of Larry Car Failures - January              210
18a      Type of Larry Car Failures - February             210a
19       Larry Car Failures - January                      211
20       Larry Car Maintenance - January                   212
21       Operating Problems - January                      212b
22       Leveler Bar Chemical Analysis                     219
23       Leveler Bar Mechanical Test Results               220
24       Partial Summary Leveler Bar Heat-Up Data          232
25       Regression Analysis - Final Leveling Bar
         Temperature                                       233
26       Summary of Leveler Bar Heat-Up Data               247
27       Leveler Bar Correlation Matrix for Midel          248
28       Distribution and Size of Suspended Solids in Tar  286b
                               IX

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                          ACKNOWLEDGMENTS

    It is not possible to acknowledge all the names of the many
individuals who willingly gave of their time and made contributions
to the project.  Dr. T. E. Dancy* directed the early development
work at J&L Steel involving J. J. Butler and J. P. Connolly.
Engineering work by Koppers Company was the responsibility of
S. P. Resko and L. G. Tucker.

    Major contributions to this AISI program were made by members
of the Joint Coordinating Group on Coke Plant Equipment under the
Chairmanship of F. C. Lauer, Assistant Works Manager, Aliquippa
Works, J&L Steel.  This chairmanship is now held by J. G. Munson,
Jr., U. S. Steel Corporation.  Mr. R. L. Dobson, Wheeling-Pittsburgh
Steel, as Chairman of the Technical Committee on Coke Oven Practice,
was actively involved.  The advice of W. M. Smith in the area of
emission and environmental testing is acknowledged.

    Dr. E. O. Kirkendall, Vice President, AISI, was the Project
Director and responsible for all work performed on this contract
with the Federal Government.  The interests of the Environmental
Protection Agency, in helping with the development of a smokeless
charging system, were represented by N. Plaks and R. V. Hendriks.
    The project at Jones & Laughlin was under the management of
W. G. Ulevich.  Test work atP-4 Battery involved the close
cooperation of the By-Product Department and the help given by
T. R. Greer, Superintendent, was appreciated.  The direct
supervision of the work on P-4 Battery was the responsibility of
J. R. Lee whose many contributions helped bring about an operable
system.  He was succeeded by T. G. Szczepanski, whose oven
experience was utilized in solving operating system problems.

    Particular thanks are due J&L personnel L. J. Tyrrell,
Maintenance; A. A. Mammarelli, Environmental Control; E. C. Renninger
and G. W. Kiefer, Operations; J. L. Kiefer, Chief Chemist;
J. L. Sundholm and R. W. Helm, Engineering; C. E. Earth, Electrical
Maintenance;     N. C. DeLuca, E. A. Mizikar, L. S.  Pope,  and
R. M. Patalsky, Research; and B. A. Zemke, Development Engineering.


    *  T. E. Dancy   Now with Sidbec - Dosco, Montreal, Canada

                                x

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    The work done on this system would not have been possible
without the engineering by Koppers Company.  This portion of the
project was managed by W. D. Edgar.  The work of Koppers engineers
H. R. Bartlebaugh, larry car design, and E. C. Hetrick  is
acknowledged.

    The larry car cab and control room and the electrical systan
were furnished by General Electric.

    And a final note of appreciation is due Jane Mattes, who typed
the many required reports in addition to this final one.  Milan
Mrkobrad made all the sketches.

    The work upon which this publication is based was performed
pursuant to Contract No. CPA-70-162 with the Environmental
Protection Agency.
                                      J.  H.  Stoltz
                                      Project Supervisor
                                XI

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                           SECTION I

                          CONCLUSIONS

    A full scale demonstration of a coke oven charging system
designed to meet future air pollution standards was engineered,
built, installed, and tested on an existing battery with a single
gas collecting main. A one year test program was included to
permit design modifications to be made where necessary to
improve system reliability.  Specific test procedures were used
in making an evaluation of the charging emissions and equipment
reliability.

CHARGING EMISSIONS

    The system was to reduce emissions sufficiently to meet  future
air pollution control regulations. The quantitative evaluation
of emissions was determined visually according to the number of
seconds the charging emissions correspond to a given Ringelmann
number or equivalent opacity.

    After a year's operation, it can be concluded that the present
system has resulted in a significant reduction in emissions dur-
ing charging when compared with the results using conventional
charging cars at P-4 battery.  A direct comparison of results can
be made from Figure 1 which shows average emissions from the new
P-5 larry car.  Similar data for the P-3 conventional table  feed
larry car is shown on Figure 2.  The data, taken by the emission
control engineer, is presented in terms of opacity.

    In spite of this improvement, the average charging emissions
have not been reduced to a level that will meet the minimum
acceptable criteria for this project, nor will they meet the local
air pollution control regulations  now applicable to P-4 battery.
Table 1 compares the emissions which occur during charging with
the various air pollution criteria..  The emission data presented
represents the best results that can be reasonably expected when
all components are functioning properly.

    There have been a few smokeless charges made with this
system, but they represent the exception to normal performance.
It has not been possible to make smokeless charges consistently

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N)
     (ft
     0
     t)
ISO
140
130
120
110
100
 90
 80
 7O
 GO
 so
 40
 so
 20
 10
                     COKE OVEM
                                O15SERVAT1OUS
                                   S POR, U
                  WITH AlSil/ErPA
DATE-. OCT.   ,1973
                                       OPACI'TV As A FuudTtcm Of
                                                         TIM&
                                                   GO
                                                    80
                        OPACITY , percent
                                    1

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 (ft
^
 o
 o
 o
 (0
ISO
140
130
120
no
100
 9.0
 80
 70
 60
 50
 40
 30
 20
 10
                 COKE, OV&N
                                                  DATE: OCT. 1973
                                 FOR 2O
WITH' P -3 TATTLE,
                                                 L-ARRY
   A FUHCTIOK OF
                     OPACITY

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   Table 1.  LARRY CAR CHARGING EMISSIONS COMPARED WITH VARIOUS

                      ACCEPTABLE CRITERIA

                      (Single gas off-take)
Measured Parameter
Seconds
Avg. charge cycle time
Avg . TO
Avg . Tl
Avg . T2
Avg. T3
5 Charges
December
1973
258.6
68.8
85.6
71.0
37.0
Minimum
Acceptable
Criteria
for Project
Xa
X
X
^ 108b
<: 36
Local Air Eollution
Regulations
X
X
X
0
0
    a.  X - No limiting value.

    b.  Criteria values are based on 5 charges per hour.

Charge Cycle Time = Interval from start of coal charge till
                    re-lidding complete.

               TO = Number of seconds no smoke.

               Tl = Number of seconds in which smoke opacity
                    is less than 20% (Ringelmann #1) but
                    greater than TO.

               T2 = Number of seconds in which smoke opacity is
                    less than 40% (Ringelmann #2) but greater
                    than Tl.

               T3 = Number of seconds in which smoke opacity is
                    equal or greater than 40% (Ringelmann #2)
                               4

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                        SECTION I   (cont.)

because during leveling there is no way to assure an open gas
passage at the top of the oven with a single gas off-take.

ACHIEVEMENT OF SMOKELESS CHARGING

    To approach smokeless charging conditions  (any and all smoke
less than 20% opacity),  it is necessary that the system be modified
by the addition of a second gas off-take at each oven.  As
described in the section on Project Results (pg. 78), the addition
of a "jumper pipe" connecting the extra coke side smoke hole on
one pair of ovens was used to observe the effect of a double gas
off-take.  The results of fifteen charges using jumper pipes, shown
in Table 2, can be compared with the results in using a single
gas off-take in Table 1.

    Emissions equal to or exceeding 20% opacity occurred for an
average of 8.4 seconds per charge.  It may be possible to
reduce this average value somewhat as additional experience is
gained in the use of jumper pipes.

    BY PRODUCT SYSTEM

    At this time, any adverse effects of this charging system on
the By-Products appears to be minimal.  Since the raw gas from
five batteries make up the by-products, it is difficult to isolate
the effects of this charging system from the whole.  During the
past year there has been no significant change in the quality
of the tar.

    The following changes have occurred that may be attributed
to the installation of "jumper pipes" on the other four batter-
ies as well as the effect of this charging system on P-4 battery.

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  Table 2.  LARRY CAR CHARGING EMISSIONS USING A JUMPER PIPE




                      (Double gas off-take)
Measured Parameter
Seconds
Avg. charge cycle time
Avg . TO
Avg . Tl
Avg . T2
Avg . T3
15 Charges
Ja nu ar y-Ma r ch
1974
219 .5
197.6
13.5
4.0
4.4
Smokeless
Charging
X
X
X
0
0
Definition of Terms Shown Below Table 1.

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BY-PRODUCT SYSTEM  (continued)

1.  The air content of the coke oven gas has increased somewhat
    ( 20%) as evidenced by an increase in nitrogen.

2.  The sludge taken from the flushing liquor decanter tanks has
    increased about 15% during the past year.

3.  The frequency at which condensate drains requires cleaning
    has increased in the past year, and the drain tar is heavier.
    This is noticable at the primary cooler, the gas exhauster,
    the tar extractor, and the gas booster  (compressor).

4.  The result of accidentally leaving the aspirating steam on
    several ovens  (beyond the charging requirements) is to
    increase the volume of coke oven gas.  An excessive increase
    in gas will overload the primary cooler causing ah increase
    in the temperature of the gas.  This results in a correspond-
    ing increase in gas volume which, if of sufficient magnitude,
    can reach the limit of the gas exhauster.  This causes
    increased back pressure that will decrease the oven suction.

    None of these effects represents a significant problem at
this time.

CHARGING EQUIPMENT RELIABILITY

    The coal charging car and associated equipment was to achieve
sufficient reliability so as to be available for satisfactory
production operation 90% of the total scheduled operating time.
The larry car availability measured over a  three-month period
was 86.0%.  The two principal factors which limit the reliability
are:

1.  Failure of hydraulic equipment, sensors, and wiring
    principally as a result of burning gases under pressure.

2.  Failure of wet coal to reliably discharge from the hopper
    drop sleeves.

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IMPROVE WORKER ENVIRONMENT ON TOP OF BATTERY

    The environment on top of the battery was to be improved for
operating personnel.  The charging equipment was mechanized and
automated so that normal duties of the charging car operator
could be performed from within the controlled environment of an
enclosed cab.  By incorporating the functions of lidding, damper-
ing, and steam aspirating into the larry car operation,  it was
hoped that there would be no need for continually exposing any
operating personnel to the top side battery environment.  The
opening and closing of the leveler door was mechanized so that
the pusherman could operate the door from within the pusher cab,
and avoid exposure to oven flames.

Charging Car Operator's Environment

    The top battery environment of the charging car operator
has been considerably improved as a result of initiating
sequences from within an air conditioned cab.

    At the present time there are three occasions for the operator
to leave the cab.

1.  Cleans gooseneck with manual swab.

2.  After placing oven on-the-main, he usually inspects  ascension
    pipe linkage to determine proper operation.

3.  If problem arises with coal feed, he leaves cab to look
    inside hoppers, and, if necessary, he leaves the car to
    start coal flow with a steel rod at the drop sleeves.

    Manual cleaning of the gooseneck will no longer be required
if the remotely operated cleaner becomes fully operational.
The inspection of ascension pipe linkages takes only a few seconds
and represents no serious exposure.  The problem of coal feed
represents the most severe shortcoming.  With wet coal conditions
this problem may occur on about 10% of the charges.  The
operator's time outside the cab on the battery averages  less
than 15% of the total, thus representing a significant reduction
in exposure.  If improvements in the coal feed system are achieved
this figure can be cut in half.
                               8

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Lidman's Environment

    The dimensional variations of the standpipes with respect to
the larry car position has limited the reliability of the
mechanized damper and steam aspirating system.  The lidman
operates the linkages on those ovens where satisfactory mechanized
operation has not been attained.  The performance of the lid
lifters has been satisfactory and has virtually eliminated the
worst task of lidding.  However there are a few times when manual
lidding must be performed even though the mechanical lidding is
reliable and working.  The lidman must perform additional tasks
which include sealing of oven ports when necessary.

    When jumper pipes are installed on this battery, it will be
necessary for the lidman to manually operate the jumper pipe
valve and control the aspirating steam valves.  Operation of
the damper and ascension pipe lid will be done by the larry car,
utilizing the lidman only in case of a malfunction.

    The exposure of the lidman to emissions has been significantly
reduced as a result of improving charging performance,  and the
use of a lid lifter.

Pusherman's Environment

    The use of a mechanized leveler door operator has improved
the pusherman's environment as a result of operating the doors
from within the cab.  He now opens the door manually only in
case of   occasional equipment malfunction.

AUTOMATIC CHARGING

    The larry car operator was provided with two methods for
controlling the coal charging process.  The automatic mode
initiated operations according to pre-determined sequential
criteria.  The manual mode of charging was accomplished by
initiating individual sequences under the operator's direction.

    The automatic sequence was not used extensively.  The
principal problem was related to its basic design which required
successful completion of a given sequence prior to initiating

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AUTOMATIC CHARGING  (continued)

the next step.  If a sub-operation was not completed,  it was
necessary to switch to the manual mode in order to continue.

    An example is the failure of coal to flow from one of the
drop sleeves.  Under these conditions the operator closes the
butterfly valves of the unaffected hoppers, and uses a bar to
initiate proper coal flow.  He then opens all butterfly valves
and resumes normal charging.  This type of problem occurs with
sufficient frequency that makes it impractical to use  the auto-
matic mode.

    The automatic system did work when the charging equipment
performed as designed.  The signal system between the  larry car
and the pusher machine functioned properly, but the wayside loop
at the pusher machine would require relocation away from exposure
to flame to achieve acceptable reliability.

    The manual mode used in charging has sufficient flexibility
and reliability to enable an operator to use it with confidence.
The use of this manual mode appears to be an acceptable means
of charging ovens.

ENVIRONMENTAL CONTROL UNIT

    The air in the larry car cab and control room was conditioned
by an environmental control unit.  This unit was designed to
remove particulates and harmful concentrations of coal tar pitch
volatiles,  SO2, H2S, and CO from the incoming air.  It also
controlled the air temperature.

    The unit does provide the larry car operator with an
improved environment..  It has been expensive to maintain and
it failed to meet the specifications for removal of particulates,
coal tar pitch  volatiles, and CO.
                               10

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                            SECTION II

                         RECOMMENDATIONS

SMOKELESS CHARGING

    As a result of extensive test work on the single gas off-
take system, and observations using the double gas off-take
(jumper pipes),  it is recommended that a 'double gas off-take be
used so that an open gas passage at the top of the oven can be
maintained at all times during charging.  This second gas off-
take can take the form of an additional gas collecting main or
some form of a jumper pipe  (breeches pipe) arrangement.

IMPROVED SYSTEM OPERATION AND RELIABILITY

    There are two steps that must be taken to realize significant
improvements in the operation and reliability of this charging
system.

1.  Addition of second gas off-take

2.  Improved coal feed system

    The second gas off-take will minimize the incidence of
hot burning gases during charging which damage hydraulic hoses
and electrical wiring and sensors.

    It also relaxes the requirements of the coal feed system.  It
is no longer necessary that the coal feed rates be closely con-
trolled, it is required that the coal flow be reliable.  Reliable
coal feed is possible from either a forced feed system  (table or
screw feed) or a properly designed gravity feed system.

    With regards to this particular larry car gravity feed system,
improved coal feed can be obtained by either of two possible
solutions.

1.  Redesign the present gravity feed system

2.  Change to a table feed system

                                 11

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IMPROVED SYSTEM OPERATION AND RELIABILITY  (continued)

    The less costly alternate of redesigning the present gravity
feed system is preferred, if this can be successfully accomplished
Since the necessary redesign may involve only a modification of
the drop sleeve, without affecting the hydraulic or  electrical
systems, this alternate solution  will  be given a first trial.
The change to a table feeder system would  represent  a major under-
taking.

    The addition of the jumper pipes and the accomplishment of
a reliable coal feed system is expected to result  in a  larry car
availability of about 95%.

    There are several general considerations that  can be followed
to improve the over-all system reliability:

1.  Design mechanical equipment that will  function properly with
    the large dimensional variations that  exist on a battery.

2.  Decrease the exposure of electrical equipment  to the battery
    environment by minimizing the number of sensors  and length of
    conduit runs, and adequately protecting required sensors.

3.  Reduce hydraulic leakage by minimizing and shortening hose
    lengths.

IMPROVED WORKER ENVIRONMENT

    It does not appear feasible to eliminate the need for
exposure of operating personnel to the top side battery environ-
ment.  Even if the larry car performed all functions of lidding,
dampering, and steam aspirating, the following tasks would still
be required.

1.  Maintain cleanliness on the battery top

2.  Remove carbon from charging holes and  standpipes

3.  Wet seal oven ports as required

4.  Watch for malfunctions

                               12

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IMPROVED WORKER ENVIRONMENT  (continued)

    It must be recognized that the top battery environment is
being continually improved not only from smokeless charging, but
also from reduced door leakage and improved pushing techniques.

AUTOMATION FOR COKE OVEN CHARGING

    A large amount of automation was provided for this prototype
system to accomplish two principal purposes:

1.  Charge ovens in a controlled sequence that would minimize
    emissions.

2.  Remove operating personnel from continual exposure to the top
    battery environment.

    It is now apparent that  smokeless charging can be accomplished
on a modified system under the control of an operator using the
manual operating mode.  It is doubtful if the need for a lidman
could be eliminated with a working automatic system.

    The use of an automatic  system requires for successful per-
formance:

1.  Reliable operation of all mechanized equipment so that the
    automatic system can remain in continual operation.

2.  Trained technicians that will maintain it in operation.

3.  Return on investment by  improved results.

    The two objectives which prompted the selection of an automatic
system have almost been as substantially satisfied by the present
manual operating mode as would be possible with a working automatic
system.  It seems unlikely that a reasonable return would be possible
using an automatic system, and consequently its use is not recommend-
ed.

APPLICATION TO NEW OR EXISTING BATTERIES

    The application of this modified charging system can be considered
                               13

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APPLICATION TO NEW OR EXISTING BATTERIES  (continued)

for use on new or existing batteries where a double gas off-take
exists or can be provided.
                               14

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                           SECTION III

                           INTRODUCTION

    Metallurgical coke, used in blast furnace  iron production,  is
made in slot type ovens by the controlled heating of coal.  The
coal is poured into hot ovens through charging holes from coal
hoppers of a larry car that travels on rails over the top of the
battery.  Charging emissions, consisting of hot gases and
particulates, result from the release of volatile matter within
the coal.  The use of steam jets in the ascension pipes connect-
ing the oven to the raw gas collecting main helps direct most of
the charging emissions into the closed .by-product system.  This
is known as charging on-the-main.  Not all the emissions are
directed into the gas collecting main and a significant portion
are released to the atmosphere through open charging holes and
empty feed hoppers (Figure 3, 4).  Additional emissions occur
during the coking cycle as a result of door leakage and when the
coke is finally pushed from the oven and quenched.  Estimates
indicate that charging emissions represent 50-60% of the total.
Coke oven air pollution is a source of concern to the community
as well as industry.

PROJECT - CONTROL CHARGING EMISSIONS

    The American Iron and Steel Institute has made studies over a
number of years addressed to the environmental health problems
associated with coke oven emissions.  The results of these early
studies led most steel companies to initiate programs related to
control of coke oven emissions.

    In 1967 Jones & Laughlin started development work on a charg-
ing system that would meet future air pollution control standards. The
results of this investigation favored the concept of controlling
the flow of oven gases 'and particulates generated during charging
so that they preferentially enter the gas collecting main.  This
technique was not new.  Development of this method had been report-
ed at batteries in England3,  Germany4, and the Soviet Union5.

    This concept was discussed with the AISI Joint Coordinating
Group on Coke Plant Equipment which had been conducting an independ-
ent investigation into improved charging methods.  This committee
had concluded that the concept of using gas cleaning equipment on
the charging car was not likely to achieve an acceptable level of

                               15

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EMISSIONS - CONVENTIONAL CHARGING
CHARGING OVEN WITH CONVENTIONAL
     GRAVITY FEED LARRY CAR
           FIGURE 3
              16

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EMISSIONS - CONVENTIONAL CHARGING
   OVEN TO BE RELIDDED AFTER
  CHARGING COAL WITH LARRY CAR
           FIGURE 4
              17

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PROJECT - CONTROL CHARGING EMISSIONS  (continued)

air quality.  The AISI accordingly decided to support development
of an oven charging system based on controlling oven pressure.  In
March, 1969 a contract was signed whereby Jones & Laughlin Steel
Corporation would manage the AISI coke oven charging study, with
engineering work performed by Koppers Company.

    A general specification was prepared which outlined the
requirements of the new charging system.  The equipment necessary
to build a prototype production model was described.  Test programs
were set up for equipment evaluation.

    In 1970 the AISI recommended joint sponsorship of construction
and testing a full-scale production prototype coke oven charging
system at P-4 Battery of the Jones & Laughlin Pittsburgh Works.
Negotiations with the United States Government represented by
the  Environmental   Protection   Agency  resulted in a  contract
being   signed  effective   June 30,  1970.    Under the terms  of
this   agreement   the  government shares half the cost of this
project  with  the  AISI.    Upon  completion  of the  produc-
tion prototype testing Jones & Laughlin will reimburse the AISI
and the U.S. Government in accordance with the depreciated value
of the economically operable equipment.

PROJECT GOALS

    The object of this program was to demonstrate a full-scale
operable charging system with the following features:

1.  The system was to perform reliably and achieve a significant
    reduction in charging emissions.  It was to have no adverse
    affect on the by-products.

2.  The environment on- top of the battery was to be improved for
    operating personnel.   The equipment was to be mechanized and
    automated so that normal operations could be performed from
    within an enclosed cab, thus eliminating the need for continual
    exposure of operating personnel to the top side battery
    environment.

    Production testing was required to determine the extent to

                                18

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PROJECT GOALS  (continued)

which project goals were achieved, and to make necessary equip-
ment changes for the realization of these goals.  This work was
performed according to an organized plan which outlined the type
of testing intended to establish the reliability of the larry car
and associated charging equipment.  Criteria were established for
judging the success in reducing charging emissions.

PROJECT COSTS

    The total appropriation was $1,877,040.00.  The project was
completed within that cost.
                               19

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                            SECTION IV

                   AISI/EPA COAL CHARGING SYSTEM

CONCEPT

    In concept the AISI/EPA Coal Charging System  eliminates
emissions during charging by causing all the oven gases  to pass
through the ascension pipe into the gas collecting main  (Figure
5).  This requires the use of an ascension pipe steam  ejector
that is capable of delivering a volume of gas equal  to that being
generated and displaced during charging.  The resulting  low
pressure  (atmospheric or slight vacuum) creates a tendency at
oven ports for air to be drawn into the oven.

    This oven pressure control concept requires, as  an essential
part of the system, that all oven ports be sealed.   During
charging the leakage of air into the ovens must be limited so as
not to significantly affect the quantity and quality of  raw gas
entering the collecting main particularly with respect to safe
levels of oxygen.  If during any part of the charging  cycle, the
quantity of gases generated exceeds the capacity of  the  ascension
pipe steam ejector, emissions during the short interval  would not
be significant.  A passage across the top of the oven  to the
ascension pipe must be assured to permit free flow of  gases, thus
minimizing pressure build-up.  These conditions must be  satisfied
with a suitably controlled coal feed and leveler bar operation.
At the end of coal charging, the equipment for sealing oven ports
is retracted sequentially as required to prevent emissions.

CHARGING EQUIPMENT

    The components provided for this system are shown  in Figure 6.
The equipment consists primarily of a new larry car, modifications
to an existing pusher machine, and additions to the  battery-

Gravity Feed Coal Charging Car

    A gravity feed system was selected for this car.   A  drop sleeve
underneath each hopper is lowered to seat within the charging hole
ring prior to charging coal into the oven.  A butterfly  valve at
                                20

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                  COKE OVEN CHARGING SYSTEM
                     SINGLE GAS OFF-TAKE
FEED HOPPER
WITH;
SHUTOFF VALVE
                            FIGURE 5
                              21

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              AISI CHARGING SYSTEM AUTOMATION
                                                         r^i
                                                         * ""^ i
b. LEVELER BAR                   i. LEVELER DOOR OPERATOR
c. UHF ALIGNMENT DEVICE           j. LEVELER DOOR SMOKE SEAL
d. ASCENSION PIPE DAMPER ACTUATOR  k. BUTTERFLY VALVES
e. GOOSENECK CLEANER             I. CONTROLLED ENVIRONMENT CAB
f. ASCENSION PIPE ACTUATOR         m. COAL HOPPER
  (PLACE OVEN-ON-MAIN)            x. OVEN TO BE CHARGED
g. LID LIFTERS                    y. OVEN TO BE PUSHED
h. FEED HOPPER DROP SLEEVES       z. OVEN TO BE DAMPERED-OFF

                          FIGURE 6
                             22

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Gravity Feed Cpal Charging Car  (continued)

the bottom of the drop sleeve is oscillated to control the rate of
coal feed.  Coal level sensors determine the initiation of level-
ing and the final termination of coal feed.  Sufficient coal is
left in the drop sleeve to form a coal seal.

    Mechanized lid lifters remove and replace lids.  The operation
of the ascension pipe damper valve, standpipe cap, and steam
valve is controlled from the larry car by the operation of two
rotary actuated  levers.  One lever raises  to  place the oven on-
the-main by turning on aspirating steam, opening the damper, and
closing the cap.  The other lever lowers to damper off the oven
by closing the damper valve and opening the stand.pipe cap.  A
remotely operated car mounted gooseneck cleaner, with motor driven
flails,cleans the gooseneck and return bend as it moves through the
standpipe inspection port.

    This equipment is powered from a central hydraulic system.
Movement of the various mechanisms must be related to the larry
car position on the battery with respect to a given oven.  An
automatic positioning system was furnished to accurately stop the
car at the proper oven charging reference position.  A special
UHF interlock system was provided to assure that the pusher
machine and the charging car were aligned on the same oven prior
to charging.

    The car was designed so that all charging operations could
be initiated by the operator from within an enclosed cab.  An
environmental control unit furnishes clean temperature controlled
air.

    The operator was provided with an automatic and a manual means
of charging ovens.  The automatic mode ensured that a definite
sequence was followed during charging to minimize emissions.  The
manual mode, under the control of the operator, did not require
any control signal interlocks with the pusher machine.

Pusher Machine Equipment

    The necessary modifications to the existing P-4 pusher machine

                               23

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Pusher Machine Equipment   (continued)

included the relocation of the leveler bar with  respect  to the
pusher ram so that ovens could normally be pushed  and  charged
without moving the pusher machine.  A new light  weight self-
supporting leveler bar was provided so that leveling   could be
initiated shortly after the start of charging.   A  smoke  seal
around the leveler bar seals the door opening during charging.

    A mechanized leveler door operator permits the pusherman to
close and open doors from within the cab.

Battery Modifications

    The required steam aspirating performance necessitated the use
of high pressure steam.  Accordingly a  new steam line was built with
provisions for regulating pressure.  Self cleaning steam nozzles
were provided to assure the maintenance of a properly  directed
steam jet.  Five new goosenecks were installed having  improved
gas flow characteristics.  A corresponding increase in gas flow
through the existing goosenecks was obtained by  increasing the
steam nozzle size.

    The addition of linkages at each ascension pipe was  required
to permit remote operation of the damper valve,  standpipe cap,
and steam valve.  It was necessary to relocate charging  hole rings
to permit proper seating of the la rry car drop sleeves.

    Panels with brass vanes were mounted at each oven  for the
larry car positioning system.  It was necessary  to reinforce the
collector rail supports on which they were mounted.  Other portions
of the battery were reinforced to hold the additional  weight of
the larry car.

    A way-side loop antenna was installed the length of  the
battery for the larry car, and one for the pusher machine,  as
required by the signal system.

AUTOMATIC CHARGING SEQUENCE

    A complete  charging sequence in the AUTOMATIC mode will

                               24

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AUTOMATIC CHARGING SEQUENCE  (continued)

describe the original intended operating procedure by reference
to Figure 6.

1.  The car hoppers are filled with a specific coal volume determin-
    ed by the measuring sleeve setting on each hopper.

2.  The car is manually moved to within one oven space north of
    the next oven to be charged  (x).

3.  At about the same time, the pusher machine operator removes
    the pusher side door from the next oven to be pushed  (y) and
    then positions the machine for single spot pushing and leveling
    (the oven to be pushed is two ovens south of the one to be
    charged).

4.  Normally the leveler door will be open and the pusher operator
    will advance the leveler bar  (b) until the leveler boot seal
    (j) is positioned over the .door opening.  This results in a
    signal to the coal charging car indicating "leveler boot
    extended".

5.  Meanwhile the charging car operator actuates the AUTO CHARGE
    pushbutton.

    The car will automatically move south and stop within _+ 0.35"
    of the oven to be charged.

    a.  Normally the lids of the oven to be charged will have been
        removed.  If the pusher machine operator had not previously
        brought the leveler boot seal to the oven (step 4) the
        oven lids are replaced so that the butterfly valves (k)
        are not exposed to the oven heat while waiting.

        The ascension pipe cleaner (d) removes carbon from the
        standpipe located two ovens south of the one to be charged.
        The cycle is then halted until the leveler boot is extended,

    b.  With the leveler boot extended an alignment check is made
        to determine that the two machines are ready to charge the

                               25

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AUTOMATIC CHARGING SEQUENCE  (continued)

    b.   (continued)
         same oven.  A UHF transmitted signal  (c)  from  the pusher
         is detected by the receiver on the charging car.

6.  With an affirmative alignment check, three simultaneous
    operations are initiated.

    a.   The lids that remain on the oven charging holes are
         removed by automatic lid lifters (g) and  set down on  the
         battery.  After these lids are removed, the feed hopper
         drop sleeves  (h) are lowered down over the charging hole
         to seal the openings.

    b.   A rotary actuator on the car operates the ascension pipe
         linkage (f) so that the steam is turned on, the ascension
         pipe cap is closed, and the damper valve  is opened.

    c.   If the gooseneck (two ovens south)  had not been previously
         cleaned, (step 5-a),  this is done now.

7.  The  previous steps complete the preparations  required prior to
    the  actual coal charging.  When all these operations have been
    completed, the three hopper butterfly valves  open  and start
    oscillating (k).  This can be done simultaneously  or with
    selective time delay.  When a level sensor detects that 75%
    of the hopper coal load has been charged into the  oven, the
    butterfly valve is closed.  After all three butterfly valves
    are closed, a request is transmitted to the pusher to start
    leveling.

8.  As soon as the first butterfly valve closes (100%  coal charge),
    the re-lid cycle s-tarts.   Charging hole lids  are replaced
    sequentially in the order of closing so that  only  one open
    charging hole can exist at one time.

9.  When all three butterfly valves are closed, a request is made
    to the pusher to start the final leveling pass.  This causes
    the leveler bar to make one complete final pass and retract
    to a point just inside the leveler door.

                                26

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AUTOMATIC CHARGING SEQUENCE  (continued)

10.  After the re-lid operation is complete, the pusher machine
     is requested to retract the leveler bar.  The pusher operator
     then actuates a pushbutton which causes the automatic leveler
     door actuator to close and latch the leveler door.

11.  Upon receiving a signal that the leveler door is closed and
     latched, the ascension pipe steam valve is closed and the
     charging cycle is complete.

12.  The operator then manually traverses the car almost two oven
     spaces south and actuates the REMOVE LID pushbutton.  This
     causes the charging car to spot on the oven that just was
     or is now to be pushed  (located two spaces south of the one
     just charged).

13.  After the car is spotted the lid lifters remove one or more
     pre-selected lids so that decarbonizing of the charging holes
     takes place.

14.  The car also closes the damper and opens the ascension pipe
     lid on the oven four spaces south of the one just charged (Z).
     This results in decarbonizing of the standpipe.  The operator
     then returns to the coal bin and the total cycle is completed.

MANUAL CHARGING SEQUENCE

    The manual mode permits considerable flexibility in the charg-
ing sequence.  There are no control interlocks between the larry
car and pusher machine.  A voice communication system permits the
operator to coordinate the charging operation.  A typical sequence
presently used (single gas off-take)  is as follows:

1.  The car hoppers are filled with a specific coal volume deter-
    mined by the measuring sleeve on each hopper.

2.  The car is moved to the oven to be charged and spotted manually
    using a visual spotting target.  After the car is properly
    positioned,  the operator pushes a CAR SPOTTED PB  which
    satisfies a requirement that the car must be positioned to
    initiate any charging functions.  The larryman operates a

                               27

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MANUAL CHARGING SEQUENCE (continued)

2.   (continued)
    pushbutton to clean the gooseneck of the oven to be pushed
     (two ovens south)  with the gooseneck cleaner.*

3.  At about the same time, the pusher machine operator removes
    the pusher side door of the oven to be pushed, and then
    positions the pusher for single spot pushing and leveling.

4.  The leveler door is opened and the pusher operator advances
    the leveler bar until its smoke seal is positioned over the
    door opening.  He then notifies the charging operator over the
    voice communication system that charging can begin.

5.  The steam on PB is operated to place the oven on-the-main by
    turning on aspirating steam, opening the damper, and closing
    the standpipe cap of the oven to be charged.

6.  The charging car drop sleeves are lowered into the open
    charging holes (one PB for each drop sleeve).

7.  The butterfly valves are opened and oscillated by operating
    the individual push buttons.

8.  The operator observes the top coal level indicators.  The
    individual lights are energized when the coal level drops
    about two feet in the hopper measuring sleeve (about 10-15
    seconds).  Vibrators are normally used at all times during
    charging.  When selected, they operate whenever the butterflies
    oscillate.  If for any reason the coal flow does not start
    in a particular hopper, the operator uses a bar to get it
    started.

9.  The operator stops the coal flow at #1 and #2 hoppers as the
    respective 75% coal charged lights turn ON.  #3 hopper con-
    tinues to empty.
      This assumes successful use of the hydraulically operated
      gooseneck cleaner scheduled for installation  March  ,1974.

                               28

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MANUAL CHARGING SEQUENCE  (continued)

10.  The larryman notifies the pusher operator to start leveling
     when the first 75% coal level light turns ON, provided the
     top level indicators show that coal flow has started from
     all hoppers.  If for any reason coal flow has not started
     from a hopper, he initiates leveling after the 75% coal
     charge level is indicated on all three hoppers,

11.  As soon as the pusherman notifies the larryman that leveling
     has started, the #1 and #2 butterfly valve pushbuttons are
     operated to resume oscillation and complete the coal charge.
     As the hoppers empty, bottom level detectors automatically
     close the respective butterfly valves.

12.  After all three hoppers are empty, the larryman notifies the
     pusherman, who makes the final leveler passes before retract-
     ing the bar and closing the leveler door.

13.  The pusherman tells the larryman when the leveler door is
     closed so that sequential re-lidding  (1-2-3) of charging
     holes is completed.  (Operates HOPPER RAISE PB, then REPLACE
     LID PB for each hopper).

14.  The operator uses E-Travel PB to retract the lever arm with-
     out turning OFF the aspirating steam and moves the car two
     oven spaces south and spots the car.  The aspirating steam
     is left on the charged oven to protect the larry car when
     part of it is spotted over the charged oven during this next
     operation.

15.  The oven that is next to be pushed in this series is dampered
     OFF (DAMPER PB) and the lids of the oven just pushed are
     removed (REPLACE LID PBs)  to decarbonize the charging holes.

16.  The car returns to the coal bin, and the lidman turns off
     aspirating steam of the oven just charged.
                                29

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                             SECTION  V

                   CHARGING EQUIPMENT DESCRIPTION

 GRAVITY FEED LARRY CAR

     The prototype  equipment built  was designed to satisfy the
 requirements of  this  system at  P-4 Battery (Figure 7).   This
 battery consists of 79 ovens of Koppers  -  Becker underjet design
 with a  single collecting main on the pusher side.  The  ovens are
 rated 693  ft3 with hot dimensions  of 13' - 2 1/2" high,  12'- 2  1/2"
 to  the  coal  line,  43'  - 11" long,  and 16 5/8" average width with
 a 3 1/2" taper.  Figure 8 shows a  cross  section through the battery,

     The design of  the  gravity feed larry car is shown on Figure 9
 and 10.  Based on  the  results of hopper  design research by U. S.
 Steel the  main hopper  was built with a 67° bin angle and a 24 inch
 diameter opening.   A drop sleeve underneath each hopper is lowered
 to  seat within the charging hole ring.  The drop sleeve is support-
 ed  by gimbal rings which permit lateral  movement so that proper
 seating is still achieved with  a maximum misalignment of 1 1/2"
 with respect to  the charging hole  ring.

     The bottom of  the  drop sleeve  contains a butterfly  valve
 which oscillates approximately  45° in a  cylindrical section to
 control the  coal feed  and feed  rate.  The  rate of coal  feed is a
 function of  hydraulic  pressure  and the angle of oscillation.
 The  dimensional  design of the drop sleeve  with respect  to the
 hopper  cylinder  assures a coal  seal at all times during  charging.
 A rotating eccentric vibrator is mounted on the conical  portion
 of  each hopper to  assist with the  coal feed.

     The butterfly  valve and drop sleeve  motions are hydraulically
 powered.   In the event of a hydraulic failure, return springs
 were  provided  to raise' the drop sleeve sufficiently to  clear the
 charging holes.  The operating  positions of the drop sleeve feeder
 are  shown  in Figure 11.

 Hopper Coal  Level  Control

    Three  coal level indicators were furnished for  each  hopper.
A top level  sensor  indicates  by a  visual light that the  hopper

                                30

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                  AISI/EPA LARRY CAR
VIEW FROM SOUTH END OF LARRY CAR DURING A CHARGE, BUT PRIOR
TO START OF LEVELING.
                       FIGURE 7
                          31

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                                  10

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-------
 Hopper Coal Level Control (continued)

 has been filled with coal.   It also tells the operator that the
 coal has started to discharge from the hopper at the beginning
 of the charging cycle.

     A second coal level sensor indicates  when approximately 75%
 of the coal charge is  in the oven.  With manual sequencing the
 operator closes the butterfly valve and requests leveling to
 start.   With automatic  sequencing this sensor causes the
 butterfly valve to close,  and after all three hoppers have reach-
 ed this level,  the larry car signals the  pusher to start leveling.

     A third coal level  sensor indicates when the hopper has
 emptied and causes the  butterfly valve to close with a 15" coal
 seal remaining.  The closing of the butterfly is initiated
 directly from the sensor regardless of whether manual or automatic
 sequence was used.

     The original level  sensor selected was a paddle wheel motor
 driven  device which rotates  in the absence of coal.  This unit
 is furnished by Monitor Mfg. by the name  "Bin-0-Matic".   The
 approximate hopper location  for these devices is shown in Figure
 9.

 Automatic Lid Lifters

     Automatic lid lifters  are provided to REMOVE and REPLACE lids
 (Figure 12).   Each lid  lifter consists of a magnet which is
 moved vertically and  horizontally by two  hydraulic cylinders.
 When lids are removed,  they  are placed on the battery to permit
 decarbonization of charging  holes.   To effect a proper oven seal
 when replacing  lids,  they  are oscillated  30° for about four cycles.
A  hydraulic driven rotary  actuator pulls  and pushes the oscillat-
 ing  links attached to the  magnet.   Bottom pins on the magnet
 engage  radial grooves in the lid to provide for positive motion.

     In  case of   a  hydraulic failure,  a pair of return springs
will  raise  the  lid lifter  sufficiently to clear the charging hole.
                               36

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Automatic Lid Lifters  (continued)

    The  following  sequence  occurs  when removing lids:   lid
 lifter extends,  lowers to charging hole,  turns magnet  ON,  raises
 (picks up  lid),  retracts, lowers,  turns magnet OFF (lid now on
 battery),  raises to  the travel  position.

    The  following  sequence  is  followed when replacing  lids:  lid
 lifter lowers,  turns on magnet,  raises (picks up lid from
 battery), extends,  lowers (lid  now  placed  in charging hole ring),
 oscillates the  lid over an  arc  of  about 30 ° to seal the lid,
 turns magnet  OFF,  raises and retracts to  the travel position.

    Individual  REMOVE LID and  REPLACE LID push buttons are
 provided for  each  lid lifter.   Sensors monitor all movements
 which must occur in  sequence or the cycle will stop, causing
 a  buzzer to sound  and an annunciator alerts the operator that  the
 cycle is not  complete.  Indicating lights monitor the  actuation
 of all sensors  to  help the  operator identify the incomplete
 sequence.   A  special emergency  manual switch which bypasses the
 sequence sensors is  provided to permit any single motion of
 any or all lid  lifters. This  control arrangement has  proved to
 be very  effective  and is well  accepted by the operators.
Damper, Steam Valve, and Standpipe Cap Operating Linkages

     Prior  to charging,  it  is necessary  to place the oven "on-the-
                                 36A

-------
                     AUTOMATIC  L/ID  LIFTE,R
0)
                                                             L iMIT SWITCH
                                                              'oven.

                                                                  $f>KIU(i

-------
 Damper,  Steam Valve,  and  Standpipe Cap Operating Linkages (cont-
inued)
main".  This  consists of  opening  the  steam  valve,  closing the
 standpipe cap, and opening  the damper valve.  After  the  oven  is
 charged, the  steam is turned off.   Prior  to pushing  the  coke,
 the oven is dampered off.   This consists  of closing  the  damper
 valve, allowing  sufficient  time for the valve to seal with flush-
 ing liquor, and  then opening the  standpipe  cap.

    There are three linkage systems mounted to each  standpipe:
 (1) steam valve  operating mechanism,  (2)  stand pipe  cap  operating
 mechanism, and (3) pullman  damper valve operating mechanism.
 These three mechanisms  are  operated by two  rotating  lever arms
 mounted on the larry car.   One arm, lever #2, raises to  operate
 all three mechanisms to place the oven on-the-main (Figure 13).
 When lever #2 lowers, it  operates only the  steam valve linkage
 to turn off the  steam after a charge.  Lever #1  lowers to damper
 off an oven by operating  the standpipe cap  and damper valve
 mechanisms    (Figure 14).   The damper lever and  standpipe cap
 lever mounted to  the ascension pipe each travel about 40°.

    In placing the oven on-the-main with  the car  operated lever
 #2, the  first 24° travel  of the damper lever  in  the  up direction
 will open the damper valve. The  standpipe  cap will  not  start
 closing until its lever has travelled about 16°.  The steam is
 also being turned ON during this  operation  so that sufficient
 steam is present to prevent any appearance  of coke oven  gas.
 After the oven is charged,  the steam  is turned off by lowering
 lever #2.  The energized  electro-magnet attached to  the  lever
 will pull the shoe plate  down with it. The counterweight attached
 to the damper valve mechanism, being  in the "over-center" UP
 position will hold the  damper open.   The  standpipe cap will remain
 closed,  since it requires a downward  lever  force to  open.   If
 desired by the operator the lever can be  lowered without turning
 off the  steam.  An EMERGENCY TRAVEL sequence will lower  the arm
 without energizing the  magnet.  The steam linkage remains in place.

    When the  oven is to be  dampered-off,  the car operated lever
 #1 rotates in a  DOWN direction under  a minimal hydraulic pressure.
 This will contact the damper lever and rotate it 16°.  At this
 point the car operated  lever #1 will  contact  the standpipe cap
 lever, which  causes lever #1 to stall. The damper arm

                                38

-------
gJ /I saedsfotJ Ftps-
              IVTA.IKL

-------
                              OVEM
o
                                    0. COAL CHAKCf/M
-------
Damper, Steam Valve, and Standpipe  Cap  Operating Linkages  (cont-
 inued)"~      "

 counterweight  is  now past  the  neutral point and should fall free
 the  remaining  24° of   travel  thus  closing the Pullman damper.
 After  a preset time delay  from actuation of lever #1, normal
 hydraulic  pressure  is  applied  which provides sufficient force to
 cause  the  standpipe cap lever  to  be moved through its final 24°
 travel, thus opening the standpipe  cap.  The purpose of the time
 delay  is to permit  the Pullman damper to fill sufficiently with
 flushing liquor to  prevent the coke oven gas in the collecting main
 from being discharged  through  the standpipe cap opening.
Gooseneck Cleaner

    A mechanized cleaner permitted  an  operator to control  the clean-
 ing of goosenecks by  initiating  the  sequence  from within the cab.
The original device  shown on Figure 15 consists of  rotating flails
mounted on a shaft direct driven by a  motor.   The cleaner mechanism
is  powered by two hydraulic  cylinders.   The  positioning cylinder
moves the cleaner from the travel position until the guide frame
rests in the gooseneck inspection cap  opening.   The extend
cylinder then causes the drive  head to enter  in a circular path
to  get past the opening after which it extends to its maximum
stroke before retracting.

Coal Bin Gate Operator

    A hydraulically driven coal bin gate  operator permits the
sequence of loading the larry carat the  coal  bin to be initiated
from within the cab.

Traction Drj.ve

    The traction drive is controlled from a common  thyristor
power supply which supports two independently driven 10-horsepower
mill-type motors.  The mechanical arrangement can be seen in
Figure 9,  The drive system has  low  backlash to permit accurate
car positioning.  The speed regulated  drive has a maximum speed
of 400 FPM but can be controlled at 2% rated  speed  for accurate
spotting over a charging hole.

                                41

-------
             ASCEKLSIOTst  :PlPEr
to
                                                                COAL
                                            VIE.TAT SHOWIM:C} POSITIONS
                                            OF CiaE-AMiM  MACHIME,

-------
Coal Charging Car Positioning System

     This  charging  system  requires  accurate spotting of the coal
 charging  car  over  the oven  in order  to effect a tight seal
 between the hoppers  and charging holes.   Accurate positioning
 is  also required for use  of the ascension pipe cleaner,  the
 damper actuating levers,  and lid lifters.

     An automatic spotting system was provided so that the car
 would be  automatically positioned.   The  system is designed to
 position  the  car within a band of  0.35".   Because the sensing
 position  vane switches operate with  a repetitive accuracy of
 of  _+ 0.1", the  stopping band (position and indication)  is 0.75".
 The car is manually  brought to within 46"  north of the oven to
 be  charged.   A  pushbutton operation  then initiates the positioning
 within +_  0.35".  Position is sensed  by vane limit switches which
 move over brass vanes.  Actuation  of these limits cause  the car
 to  position as  shown in Figure 16.   These  special static switches
 were furnished  by  G.E. in a water  tight  enclosure.

     The larry car  movable carriage  (Figure 17)  held the  limits
 at  a fixed position  with  respect to  the  stationary vanes on the
 battery by means of  a wheel which  rode on  an angle above the
 vanes.  The arm which attached the carriage to the larry car
 permitted variations between the position  of the car (vertical
 and horizontal) and  the brass vanes,  but maintained a fixed
 position  in the direction of larry car travel.

Hydraulic  System

     The hydraulic  system  provides  the power to operate the lid
 lifters,  hopper drop sleeves, butterfly  valves,  damper,  steam
 and  standpipe cap  mechanisms, gooseneck  cleaner,  and the coal
 bin gate  operator.   There are two  pressure compensated fixed
 displacement  piston  type  pumps rated  27  GPM at 1000 psi  and
 1200 RPM.  Only one  pump  is run at a  time,  and the other one is
 on  stand-by service.  Each  pump is driven  by a 25 HP motor.   If
 the  system pressure  drops to approximately 300 psi,  the  preferred
 pump will shut down  and the stand-by  will  start running.  Part
 of  this system can be seen  in Figure  7 (page 31)
                              43

-------
    OP&RATIOH  OF  L,AR,RY CAR
                         SYSf-TSM
 CAR To
 WHE.MTH&
                                 ^ THE. CAR, SPOT
                                        AT [Q
Q
d
to
,STOP T-R/AVEL.
                                      LIMIT FX2C
                                        K/E-OUCBC To 2
                                        PX2D Is
                                       INITIATED.
        A CAR £POT ^IC^KAL LiquT Is
            WHEK PX2A AUD PX2B
          SIWCE THE, LIMITS OFBI^ATE.
             WlTHIU ±0.1", THB SBU 0 IU CJ
        IS O.75".
                   TR.AVEL  DISTAUCE,
                            «-*
                                 1G

-------
ARRAisiq

-------
Hydraulic System (continued)

    The solenoid operated hydraulic valves, flow control valves,
sequencing valves,  and pressure switches are located in enclosed
hydraulic panels.  There are three identical panels  (Figure 18)
mounted at the end of the lid lifter frames at the north end of the
car on the battery level that each contain all hydraulic valves
for one lid lifter, drop sleeve, and butterfly valve.   A fourth
panel is mounted next to the pump units and contains the hydraulic
valves for the pump units, coal bin gate operator, rotary actuators
for the ascension pipe linkages, and the gooseneck cleaner.

Environmental Control Unit

    A Buffalo Forge Company 5-ton packaged air conditioning and
environmental contro 1 unit was furnished to improve the
environmental conditions to which the larry car operator is
exposed inside the operator's cab, as well as providing a suitable
environment for the electrical controls housed inside the electrical
control room.

    The specifications for this unit limited the time weighted
average concentrations  (based on 8 hr. work day) inside the larry
car to the following:
              Coal Tar Pitch Volatiles 	0.2 mg/M
              SC-2  	  5 PPM
              H2S  	 10 PPM
              CO 	 50 PPM

    The final filter was to be designed for 99.9% removal of
particles down to  1 micron  in size.

    This was to be a once-through system, using all outside air,
to slightly pressurize the cab and heat and cool the air to main-
tain a temperature of 70°F +, 5°F in the operator's cab, and below
90°F in the electrical control room.  Tne filtered air  from the
cab was to pass through a grill into the electrical control room
and discharge out  through a weighted louvre.

    This one unit  was to handle the ventilation of both the
electrical control room  (651 ft.3) and the operator's cab  (893
ft.3), resulting in an approximate overall air change of one  per
                               46

-------
LID LIFTER AND DROP SLEEVE HYDRAULIC PANEL
               FIGURE 18
                  47

-------
Environmental Control Unit  (continued)

minute.

    The  inlet air  is drawn  through  a  bird  screen and  fixed  louver
downward to  an AAF Co. Dual Pocket  Dust  Louvre  Air  Cleaner  (65-
4 design 2)  with  an auxilliary  exhaust  system  removing  about  20%
of the  "primary  air" containing  the large  particles removed by
this  inertial type separator.  The  efficiency of the  Dust Louvre
is rated as  92%  on Dry Arizona Coarse Road Dust,  and  78% on Dry
Fine  Arizona Road  Dust.

    The  air  then discharges into a  vertically mounted replaceable
bag type cotton  filter  (AAF #2100 Dri-Pak,  Class II)  which  has
95 sq.  ft. of cloth area  (24" x  24" x 36")  and  a rated overall
efficiency of 95%  (Atmosphere Dust  Spot  Test),  and  on the order
of 90% efficiency  at 1 micron particle size.

    The  filtered air then passes through a horizontally mounted
charcoal filter  bed (AAF-1000  24"  x  24" x 8-3/4")  which contains
45 pounds of activated charcoal  for removal by  absorption of
gaseous contaminants.   (SO2» H2S).

    The air  then passes through  a cooling  coil  (6-row, copper  fin,
copper tube, direct expansion),  thence through  a 30 KW electric
heating coil.  The cooling  coil  receives its refrigerant from  a
5 ton Lintern Model #960 heavy duty industrial  compressor-condenser
unit  located adjacent to the ventilation unit on the  larry  car.

    Finally, the air passes through a backward  curved, limit load
type  fan, with a 1 1/2 hp motor,  through the ductwork into  the
operator's cab and electrical control room.

    Discharged air temperature is regulated by  a combination of a
course two-stage temperature sensor located in  the  inlet section
and a final  temperature sensor located downstream from the  fan,
inside the ductwork.

    The arrangement of the  unit  can be seen in  Figure 19.   A
view  from the top  of the larry car  (figure 20)  shows  the air inlet
the compresser cooling coils, and the air  duct  into the  cab.
                                48

-------


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-------
ENVIRONMENTAL UNIT - TOP VIEW
          FIGURE 20

-------
 Electricel System

     The  electrical  system for  the larry car furnishes the necessary
 power  and  distribution to provide adequate and reliable means of
 operating  the  electrical  equipment.   The power system (460 volt,
 3  phase, 60 Hz)  was sized to handle  two larry cars, with a maximum
 load on  one.   The design  criteria were a load of 400 amperes and
 a  maximum  in plant  line drop of 5% rated voltage.

     The  existing power system  on this battery is 250 V.D.C.  Since
 only D-C powered cars  had been used  on P-4,  it was necessary to
 provide  an additional  set of collector rails.  This arrangement
 can  be seen on Figure  20 .

     Since  the  quench tower is  located at the south end of P-4
 battery, 180 feet of power rail at the south end were stainless
 steel  "T"-bar.   The remaining  "T"-bar was plain carbon steel.

     The  460 volt supply at the larry car is  divided into two
 separate sections of a motor control center.  The first  section
 consists of equipment  that may be energized  at all times whether
 or not the car  is being operated.  This supply,  coming directly
 from the hot-rails,  feeds  a separate incoming line breaker.
 Loads    from this source  include:
 1.   Mercury lights
 2.   Environmental Control  Unit
     a)  Three  separate heaters
     b)  Air conditioning  fan and  secondary air blower
     c)  Air compressor
 3.   Hydraulic System heater
 4.   Magnet  feeder
 5.   115-volt distribution  panel

     The second section consists of equipment that moves  and  requires
 an easy method of lock-out.  The  hot-rail feed for this  portion
 goes first  to a manual  - magnetic disconnect located outside the
 operator's  cab.   This  can  be controlled from pushbuttons on the
 console,  or manually opened.   The supply from this device then
 feeds both  the traction drive  power  conversion equipment and a
 separate incoming line breaker.   Loads from  this second  breaker
 include:

1.   Hydraulic pumps  (2)
                                51

-------
Electrical System           (continued)

2.  Vibrators (3)
3.  Solenoid transformer and supply
4.  Hydraulic Pump control

    This method of load distribution has worked out very well.
The major types of electrical equipment in the control room are:
1.  Motor control center
2.  Traction drive power converter and control
3.  Sequencing logic cabinets  (one for automatic, one for manual)
4.  Output relay cabinet
5.  Magnet controller cabinet
6.  P.C.M. control cabinet

Larry Car - Pusher Machine Alignment

    An interlock system  (Figure  21) was provided  to assure that
the pusher machine and the  larry car were aligned on the same  oven
prior to  initiating a charging cycle.  The interlock consisted  of
an ultra  high frequency transmitter  (10.2 GHZ) on the pusher
machine and a similar type  receiver on the larry  car.

Coal Charging Car Operating Modes

    Two operating modes were provided for use with this  system:
AUTOMATIC and MANUAL.  In general the MANUAL mode sequenced the
motions necessary to perform anoperation such as  REMOVE  LIDS
or OPEN AND OSCILLATE BUTTERFLY  VALVES.  The AUTOMATIC mode of
operation sequenced the individual operations.   In PREPARE-TO-
FEED it would SPOT the car  over  the oven to be charged,  REMOVE
LIDS, if  necessary, then lower the DROP SLEEVES.  Simultaneously
after the car was spotted,  it would raise lever  #2 to place the
oven ON-THE-MAIN.
    The control pushbuttons  (PB)  furnished  for  use  by the  operator
were as follows:

Manual System -
1.  Remove lid PB, replace lid  PB (three  sets - one for  each lid)
2.  Steam and damper on PB,  steam off  PB, damper off PB
3.  Hopper drop sleeve up PB, down PB  (three  sets - one  for each

                                52

-------
  PUSHE/R,- CHAE^GIMG CAR ALIQNIVIE.NT
    .1
2SOV.

~D~C. J
             l-#/G
oh
         /A// TV AT-/ A/9 ^

                -^
                                       o
                                       o
                                       ooo
                                        DECEIVER ASSY. 
-------
Coal Charging Car Operating Modes  (continued)

Manual System-(continued)
3.   (continued)
     drop sleeve)
4.  Butterfly valve oscillate PB, close PB  (three sets - one  for
    each butterfly)
5.  Clean gooseneck PB.

Automatic System -
1.  Auto    Prepare-to-feed PB
2.  Auto    Feed PB
3.  Auto    Charge PB
4.  Auto    Remove lids PB

Carrier Current Signal System

    The purpose of this system is to transmit and receive control
requests and interlock signals between the coal charging car and
the pusher machine as required by the automatic system.  Refer to
the system drawing shown in Figure 22.

    The following signals are transmitted from the larry car to
the pusher:
1.  Status - Pusher is aligned
2.  Request - Initiate alignment check
3.  Alarm - Pusher not aligned
4.  Request - Start leveling
5.  Request - Make final level pass
6.  Request - Retract leveler bar
7.  Alarm - Not leveling
8.  Alarm - Communication failure

    The following signals are transmitted from the pusher to
the larry car:
1.  Status - Alignment being checked
2.  Status - Leveler Bar operating
3.  Status - Leveler bar smoke shield extended
4.  Status - Chuck door closed and latched
                                54

-------
(n
                                   LARRYCAR
                                   EQUIPM&NT
                                     CURRENT
  1G3KMZ
 _
                  RF XMTR.
                  To PUSHER*?
                   131 KHZ
                                                                  STATIONJ

                                                              OP P--4- EbATTGrRY
      MATCH i MO
      XFMR
XFMR    rrYn      ^  i~iof>fig. |  | i ~r 0-is. n g. | |  I


      LJANTENMAj        ' '   ^.  PTcK-UP  I  I
  	1 <^-OH-	(  I
  ISOO'JL- TERM IN ATI NIC;
  J500JV,  Re.S(STOR
         v. SOUTH E.MD
          OP
                      CHARQIMQ CAR'S

                      , Loop
RF
To
                                                       XMTR
                                               CAR.
                                                 KHZ
Isnrjil TERMINATING
L50CJM  ReSlSTOR
                                  TT37KHZ XMTR

                                  '(53KH2 RCVR
                                                      R.F XMTR
                                                        C-AR
                                                       I4OKHZ
                       R.F RCVR

                       PUSHER.*!
                       I&3KHZ.
RF  RCVR
   FRO M
PUSHER *l
 I55KHZ
                                                              R1=  RCVR
                                                                FROM
                                                              PuSHErR.*?
                                                               i 5.7 KHZ
RF RCVR
                                      KHZ .
                                                                       XMTR.
                                                                    I&OKHZ
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                                     To
                                  PUSHER.
                                  PUSHER
                                                                               EQUlPMt=-KlT
                                       PIgU
                                               COAL. CHAFzqtMq CAR To PUSHIMQ MACHIM&-S

-------
Carrier Current Signal System  (continued)

    The transmission  of  information  is  a  five  digit  binary code
 sent  serially.  Error detecting  is accomplished  by alternate
 transmissions  of  code and  complement.   The  receiver  is  not up-
 dated  unless the  complement  of the second message matches  that
 of  the first transmission.   If the receiver is not updated with
 a message within  a  certain pre-set time,  a  communication
 failure alarm  occurs.

    The system is designed on a  priority  basis.  The signal of
 highest priority  that becomes true is the one  that is transmitted.
 Signals of  lesser priority are not examined.   It is  possible to
 select a signal  (for  example - an alarm)  that  has the highest
 priority to be examined  periodically only  (one second out  of ten)
 so  that during the  other times the remaining signals are examined
 on a priority basis.   This  requires careful  selection of the
 priorities  but has  not limited the system.

    For example after an alignment check  was completed  the
 "leveler bar operating"  signal is examined  first.  If it is TRUE
 the other two  signals are  not seen.  However it  is known that
 if  the "leveler bar is operating" the smoke seal must be in place
 and the chuck  door  is open.  When the "leveler bar operating"
 signal is FALSE the "smokeshield in  place"  signal is checked.
 If  this signal is TRUE,  it is known  that  the chuck door must be
 open,  since it had  to be open in order  to put  the smokeshield
 in  place.   If  the smoke  shield is retracted,  then the "chuck
 door  closed" signal is examined. If no signal is TRUE,  then a
 rest  code  (code "O")  is  transmitted  so  that a  continual check
 is  made to  determine  that  the system is in  good  working order.

    The transmitter coding is such that a  "zero" logic  signal will
 send  low-shift and  a  "one"logic  signal  will send high-shift. The
 high  and low shift  frequencies will  be  +  or -  100 Hz from  the
 center frequency  of the  associated transmitter.  The receiver
 discriminator  then  reads these signals  respectively  as  + or -
 1 volt d-c.

    The system was  designed  so that  the larry  car could transmit
 signals to  either of  two pusher  machines.   A switch  in the larry
 car selects the pusher to  be used.
                               54 B

-------
Carrier Current Signal System  (continued)

    Each machine has its own transmitter  and  receiver.   The
signal information is carried by a way-side loop consisting
of a pair of parallel wires running the length of the battery
for the charging car and for the pusher machine.   The signal is
inductively coupled to the respective transmitter and receiver by
this loop.

Voice Communication System

    Two voice communication systems were  installed in the new
larry car.  One system provides direct voice  communication with
P-3 pusher, P-4 pusher, and the charging  car.   This system is used
to coordinate the charging operation between  the  pusherman and the
larryman.  The second system permits the  larryman to talk over the
existing battery communication system which includes the foreman's
office.

    The voice system performs those functions  for manual operation
that the carrier current signal system does for automatic operation.
PUSHER MACHINE

Leveler  Bar

    The original concept of the charging  system  required that  the
leveler bar be self supporting so that  it could  be  used as requir-
ed shortly after the start of charging.  Koppers determined that
the existing leveler bar used at P-4 battery would  not  be self-
supporting, when fully extended at elevated temperatures exceeding
500° F.

    A new self-supporting leveler bar was furnished which featured
the use of bulb angles for high strength  and side cut-outs to
minimize the over-all weight.

Leveler  Bar Smoke  Shield

    A smoke shield was required around  the leveler  bar  to seal

                                55

-------
Leveler Bar Smoke Shield (continued)

the leveler door port.  This smoke boot is connected to a
spillage chute which conveys the excess coal from leveling into an
existing receiving hopper.   The smoke boot and chute system were
designed to minimize the release of coal dust.

Leveler Bar Relocation

    The maintenance of existing coke production rates necessitated
that single spot pushing and leveling be used.  This required
relocation of the leveler bar to a position two oven center-line
distances away from the ram.

Leveler Door Operation

    An automatic door mechanism permits the pusher operator to
open or close the leveler door from within the operator's cab.
The required movements are powered by three air-operated cylinders
as shown in Figure 23.  All oven doors were provided with a new
type of leveler door  (Figure 24) designed for improved self-sealing
and having a cam type latch designed for operation with the new
air powered door operator.

Electrical Equipment

    Electric control equipment was furnished  for:
1.  Automatic operation of leveler bar
2.  Automatic operation of leveler door
3.  Signal system between pusher and larry car.
4.  UHF alignment interlock - transmitter
5.  Voice communicataon equipment.

BATTERY MODIFICATIONS

Steam Ejector System

    The success of the AISI/EPA coal charging system requires
the use of a- good steam aspirating system that will cause all
the emissions to pass through the gas collecting main.  Consider-
able work was done in the early phases of this test program in
developing the requirements of such a system  as described in


                               56

-------
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-------
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-------
Steam Ejector System  (continued)

the report, "Ascension Pipe Steam Ejector  Test  Program" by John
P. Connolly, dated September 14, 1970.9

    The three main parts of a typical ascension pipe consist of
the standpipe, gooseneck, and return bend.   Figure 25 shows the
existing arrangement on P-4 battery.  The  gooseneck section has
an opening for cleaning and inspecting the unit which is sealed
by the standpipe cap.  It also has a steam nozzle  which discharges
toward the collecting main.  This nozzle is installed so that it
can be easily cleaned or replaced.  The return  bend has one or
two ammonia liquor sprays which cool the gas and condense out
the heavy tars.  The return bend is sloped  to allow the liquor
to drain into the collecting main.  A liquid sealed valve is
placed at the end of the return bend and is used to damper off
the gas collecting main.

    The ascension pipe carries the gases generated during coking
from the oven chamber into the collecting  main  which runs along
the battery.

    During charging when the evolution of  volatile gases within
the ovens is at a maximum rate, it is necessary to use aspirating
steam to increase the gas flow through the  ascension pipe.

    A steam ejector can be defined as a device  in  which the kinetic
energy of the steam is imparted to the raw oven gas in the ascension
pipe to increase its velocity.  The use of  the  steam acts like a
pump to increase the gas flow.

    Considerable testing was undertaken to  analyze the performance
of the existing steam ejector and several  new designs.  As a
result of the test work briefly described  in the section on
Project Results (pgJ56') , it was determined  that the existing
design provided adequate ejector performance.   Five ascension
pipe gooseneck and return bend assemblies  (Figure  26)   having
improved ejector characteristics were installed.   This design
featured improved spray location, smooth flow geometry, and a
concentrically located steam nozzle.  These assemblies were
installed with 11/16" steam nozzles.  The  existing gooseneck
assemblies were equipped with 3/4" nozzles  to obtain equivalent
suction capabilities.
                               59

-------
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                                 i
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-------
    ASCE/MSIOM PIPE.-
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-------
Steam Ejector System  (continued)

    As a result of the test work a high pressure  steam  line  was
constructed  for use with a 180 psi, 475°F  steam supply.  A
pressure reducing station was supplied so  that the  steam
pressure could be varied.  To minimize the effects  of coal carry-
over, the steam pressure just necessary to provide  adequate  suction
would be used.  The steam pressure is usually carried at 135-140
psi.

    Another  requirement of a good steam ejector system  is a
steam nozzle that will deliver the proper  jet into  the
gooseneck to obtain optimum suction.  It is  important that the
nozzle remain free of carbon deposits so that there  is  no inter-
ference with the steam jet that would change its  direction or
otherwise constrict it.  Considerable work was done  to  develop
a self-cleaning steam nozzle similar to that shown  on Figure 27.
These nozzles were installed on all goosenecks.

    The addition of damper, steam valve, and standpipe  cap
operating linkages to each ascension pipe  was previously described.

Charging Holes

    New charging hole covers were installed  on all  charging  holes
designed for use with the automatic lid lifters.  The design
 (Figure 28)  incorporated radial grooves which permit positive
engagement by pins on the lid lifter magnet  to ensure oscillation
of the lid.  This oscillation is intended  to cut  carbon deposits
on the ring  surface, thus improving the oven port seal.

    The lid was provided with three lugs which minimize the
possibility  of it tilting in case some one stepped  on it.

Oven Alignment

    The charging hole rings had to be re-located  so  that they
were concentrically aligned with the larry car drop  sleeves.
Sufficient alignment was required to assure  reliable seating of
the sleeves within the rings.
                                 62

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                                       5T1LAM NOZ.ZrL.Er
                    /
-------
   HOL/E/-
G4-

-------
Oven Alignment   (continued)

    The mounting of a set of brass vanes  at  each oven was required
to facilitate larry car positioning.  The panels containing the
vanes were mounted on cross members attached to  the collector rail
supports.  It was necessary to reinforce  the collector rail
supports to assure a stable position.

Battery Reinforcement

    It was necessary to reinforce portions of the battery to
handle the additional weight of the larry car.   The car weighs
approximately 70 tons empty and about 87  tons full.   Since this
car is parked at the south end of the battery next to the existing
spare larry car it was necessary to reinforce that end of the
battery.  Hydraulic bumpers were installed with  a design rating
equivalent to that necessary to stop the  car at  full speed.

    The existing coal bin scale was removed  because  it could not
handle the additional weight.  It was necessary  to improve the
stability of the rails on the rail chairs by the  addition of shims.
                              65

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                           SECTION VI

              PROJECT RESULTS - SMOKELESS CHARGING

CHARGING EMISSIONS

    The application of this charging concept to a battery with a
single gas off-take did not result in smokeless charging.  Emissions
were evaluated by visual observations based on the Ringelmann
number range or the equivalent opacity.  The detailed observation
procedure is given in Appendix D.   Some tabulated results are
shown on Table 3.

    During January and February, 1973, there were 236 charges
observed representing the initial data for evaluation of
emissions.  The average results of these charges shown in Table
3 do not meet any of the acceptable criteria listed in Table 1
(pg.4).  There were 16 charges in January during which no T3
emissions occurred.  The data for those charges is shown in
Table 4.  One obvious conclusion,  after studying the available
information for all 236 charges, is that the cause of the variable
results is not apparent from the data.  Some of the best charges
shown in Table 4 occurred in spite of unfavorable conditions such
as:
1)  Failure of a drop sleeve to seat
2)  Constrictions in ascension pipe (carbon deposits)
3)  Standpipe cap leaking
4)  Heavy flare carbon in charging holes
                               66

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             Table 3.   LARRY CAR CHARGING EMISSIONS

                     (Single gas off-take)
Measured
Parameter
Seconds
Avg. charge
cycle time
Avg. charge
time
Avg . TO
Avg. Tl
Avg. T2
Avg. T3
Jan/Feb
1973
236 chg.
227.6
172.4
54.4
99.1
24.4
50.3
April
1973
125 chg.
273.5
173.0
75.1
140.3
21.8
36.3
December
1973
5 charges
p-4 pusher
258.6
149.8
68.8
85.6
71.0
37.0
December
1973
5 charges
p-3 pusher
293.6
178.2
47.2
99.2
94.4
52.8
January
1974
10 charges
8.3% moisture
235.5
193.9
70.1
82.9
38.4
51.4
Charge Time = Interval from start of coal charge till final
              coal feed (last butterfly closed)

Definition of remaining terms shown below Table 1, page 4.
                               67

-------
CHARGING EMISSIONS  (continued)

    It was established that the emissions occur while leveling
during the final 20% charge,  and also during the re-lid cycle.
Three factors indicated that this problem was not the result of
insufficient oven suction.

1.  Prior to the start of leveling, the oven suction created with
    130-140 psi steam is sufficient to prevent emissions if the
    components of the charging system are in reasonable working
    condition.

2.  The emissions do not appear to generally occur just from the
    use of the leveler bar,  but rather from a combination of its
    use and a coal peak under one of the charging holes.  The
    occurrence of emissions can usually be associated with slow
    coal feed from one of the hoppers indicating that coal is
    backed up in the charging hole and must be removed by the
    leveler bar.

3.  Improving the oven suction by increasing the steam pressure
    will not necessarily result in less emissions.  Table 5 shows
    the results of observed charges (February 5, 6, 7) in which
    the steam header pressure was changed during part of each
    day.  The average time of T3 emissions is greater for those
    charges made with the high pressure steam.  Since it is
    known from test work that oven suction at 180 psi is greater
    than that which occurs at 140 psi, the results of the data
    in Table 5 are misleading.

    These observations and data led to the conclusion that the
principal cause of emissions was the result of not maintaining
an open gas passage at the top of the oven.

STEPS TO IMPROVE CHARGING PERFORMANCE

Step 1 - Automate Leveler Bar Stroke

    The operation of the leveler bar was under the control of
the pusherman.  Accordingly the cycling of the leveler bar was
not consistent and depended on the experience of each operator.
This particularly affected the coal being leveled under #3 charg-
ing hole.  If the bar was not extended fully each cycle, or if

                               68

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                Table U.  LARRY CAR CHARGING EMISSION DATA
                      (16 beat charges - January 1973)
Date
1-5
1-5
1-5
1-5

1-5

1-5
1-5

1-16
1-16

1-16
1-18
1-18

1-18
1-18

1-22

1-29
.
Avg.
Oven
No.
2-20
3-20
2-22
3-18

2-lU

3-ll*
3-16

1-13
2-13

1-15
2-22
3-22

2-20
1-22

3-18

2-10


TO
(Sec.)
72
37
99
125

207

21*2
177

ioi*
132

106
159
132

92
122

97

15

119-9
Tl
(Sec.)
100
130
166
117

69

1*6
58

66
63

58
130
130

116
188

1*1*

185

loU.i
T2
(Sec.)
19
21
23
08

10

07
03

19


13
11
18

32
10

27

07

17.3
Chg.
time
(Sec.)
120
159
196
ll*5

177

207
171

121*
131*

132
265
228

153
207

113

163

168.1*
Chg.
cycle
time .
(Sec.)
191
188
288
250

276

295
238

189
21*1*

177
300
280

21*0
320

168

207

21*0.5
Principal
source of
emissions
#2 D.S. Seal

#2 D.S. Seal


#2, 3 D.S.
Seal
#1 D.S. Seal
#2 D.S. Seal

#2 D.S. Seal
#2 D.S. Seal

#2 D.S. Seal
#2 D.S. Seal
#2, 3 D.S.
Seal
#2 D.S. Seal
#1, 3 D.S.
Seal
#3 D.S. Seal

#2, 3 D.S.
Seal

Unfavorable i
system i
conditions

#1 D.S. 2" Open, Seated with Vibrator
#1, 2 Charge Hole Heavy Flare Carbon
Constricted Gooseneck, Standpipe Cap
Leaked
#2 D.S. 1/1*" Open, Standpipe Cap ;
Leaked 1
#1 D.S. 2.5" Open i
#1 D.S. 2.5" Open, Standpipe Cap
Leaked
#3 D.S. 0.5" Open
#2, 3 Charge Hole Carbon, Constricted
Standpipe

#1, 2 Charge Hole Heavy Flare Carbon
#3 D.S. 1" Open


#2 Charge Hole Heavy Flare Carbon

#2 Charge Hole Carbon, Gooseneck
Constricted
#2 D.S. 1*" Open, Gooseneck Constricted


D.S.  - Drop Sleeve

-------
                             Table U.   (continued)  LARRY CAR CHARGING EMISSION DATA
Date
1-15
1-16
1-18
1-22
1-29
COAL ANALYSIS
"£
U3.U
U3.66
U3.83
Ui.28
1*3.10
% Vol.
matter
32.26
32. 2h
32.28
32.23
32.26
%
Moist .
7-0
7:39
7.23
8.25
7.0
%
Fixed
carb.
60.15
60.1
59-8
60.05
59.89
%
Ash
7.59
7.66
7.92
7.72
7.85
%
Sul.
1.2U
1.2U
1.2U
1.23
1.22
Oil
PV
'ton
3.^2
3.^7
3.38
3.35
3.38
WEATHER CONDITIONS
Temp.
0F
HU.5
Uo.o
6U.O
62
30
Wind
vel.
mph
6
15 /SW
11 Af
7/SSE
6/NNW
Atm.
Press .
29.73
29.50
29.12
30.31
29.62
Precip.
	
	
	
	
snow
%
Humid
72
70
38
U5
8U
Atm.
cond.
Overcast
Sunny
Clear
Sunny
Overcast
•-J
o
Notes   1


        2

        3

        U

        5

        6
                      #2 drop sleeve  seal at  charging hole ring was a principal source of emissions
                      69$ of the time.

                      Five  occurrences of poor drop  sleeve seating with 1" or more air gap.

                      Six occurrences of extra heavy flare carbon in charging holes.

                      Three occurrences of a  constricted gooseneck or standpipe.

                      Three cases  of  standpipe cap leakage.
                      Steam pressure was  lUo psi and steam temperature was U50°F for all charges
                      except on January 29: 170 psi and 510°F.

-------
             Table 5.  LARRY CAR CHARGING EMISSIONS
                       VARIABLE STEAM PRESSURE

                       (Single gas off-take)
Measured parameter
time in seconds
No. of charges
Avg. charge cycle time
Avg. charge time
Avg . TO
Avg. Tl
Avg . T2
Avg . T3
Steam header pressure
180-190 psi
46
224
169
48.3
86.4
25.3
63.8
140-150 psi
42
234
172.5
48.2
104.1
26.8
55.0
Definition of terms shown in Glossary,  page 193.
                               71

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Step 1 - Automate Leveler Bar Stroke (continued)

an excessively long stroke was used, the coal leveled at #3 would
be significantly less that at #1 or #2.  The worst source of
emissions frequently occurred at #3 charging hole, particularly
when #3 hopper was the last one to empty.

    The operation of the leveler bar was automated so that a
consistent repeatable stroke would be used,  thus eliminating
this factor as a variable.  The leveler bar stroke was set at
9 feet to provide maximum leveling at #3 charging hole.

Step 2 -^ Increase Gas Passage Space During Leveling

    The original leveler bar had baffles between the side plates
spaced at 33" intervals.  These baffles move the coal during the
leveling operation.  The top of the baffle was about 3/4" below
the top of the side plate.  The oven roof is approximately 2"
above the leveler bar.  The presence of roof carbon could
seriously affect any available gas passage during leveling.

    The tops of the baffles were cut 2-3" to increase the
available gas passage.  The 3" cut was made on those baffles
occurring more than 20'  back from the leveler bar nose.  The
number of baffles was doubled so that the coal would be moved at
least as effectively as before.

    It was necessary to add a chain to clean the tops of baffles
when the leveler bar was withdrawn from the oven in order to
prevent a build-up of carbon.

Step 3 _ Leveler Door Closed Prior to Lidding

    It had been observed that emissions occurred during the
sequential re-lidding of oven ports prior to closing the leveler
door.  The smoke seal at the leveler  door was not tight enough
to prevent emissions with one charging hole open.  At the expense
of increased charging cycle time, the emissions during re-lidding
could be virtually eliminated by closing the leveler door first.
                               72

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Step 4 - Slow Down Final  Coal  Feed

    The rate at which coal is charged  into  an oven greatly exceeds
the rate at which it can be leveled.   To  an order of magnitude
approximation,  a feed rate of 2.5  Ft3/sec.  would  exceed the level-
ing rate by a factor of 3 to 5.

    There is no readily available  means to  vary  the coal feed
rate during charging.  In general  the  coal  feed  rate will decrease
with an increase in the butterfly  oscillation angle.  To a lesser
extent a lower setting of the hydraulic flow control valve will
decrease the feed rate for the larger  oscillation angles (more than
60°)  by slowing down the oscillation  rate.

    The angle of oscillation used  with this  feed  system is approxi-
mately 45°.  The most effective way to slow down  the coal feed
was to increase its oscillation angle during  leveling.   The control
system was modified so that when the coal reached the 75% level,
the butterfly valve oscillated between full  open  and full closed
position.  This arrangement is shown on Figure 29.   This
accomplished a slow down in the final  feed  rate.   However it also
resulted in more occurrences of packed coal  during leveling, which
resulted in a stalled butterfly valve.  During leveling the coal
will back up into a charging hole  as shown  in Figure 5 (pg.21)
for #2 charging hole.  As this coal backs up,  the cyclic closing
of the butterfly valve during the  final coal feed has a tendency
to pack the coal in the lower portion  of  the drop sleeve.
Consequently this procedure was abandoned and the oscillation
angle now remains constant during  the  entire charging interval.

REDUCTION IN CHARGING EMISSIONS

    The results of these four modifications  appear  in Table 3 for
125 charges made in April 1973.  The average charge time was
unchanged.  The charge'cycle time  increased 46 seconds as a result
of closing the leveler door prior  to re-lidding.   The incidence
of T3 emissions decreased 28%, and that of  T2 emissions by 10%.

    The significant improvement over previous results is attributed
to the early closing of the leveler door  and the use of automatic
leveling.  The modification to the leveler  bar baffles is believed
to have helped, but its effect was not easily measured.  The

                               73

-------
BUTTERFLY  OSCILLATION, AUGLE,
    FUL.L OPEN:
    FosiTiou
                            oo'
                                 Cr.os.Ei>
                                 .POSITION
         Osctl^L^ATIOH
45° SSTT Bv
SwtTCHS.
                                  OF
                            PROXIMITY
   FIMAL, OSCIUE^ATIOU AWGJUE/ OF
   AFFROXItvTAT£,L/tr 100° DETE.RMIMEX)
      FUUL. OPE.M AUD CLOSE Posirtoits.
   MlTlATlOVl OF
          Occurs WHEU COAL
         OR DETE.-R/MIKTBS  THAT 7S%
         CHARGE Is  COMPL/STEL.
                        29
                 74

-------
REDUCTION IN CHARGING EMISSIONS  (continued)

increased opening above the baffles  reduced  the effectiveness
of the leveler bar smoke seal.  As previously indicated the
butterfly angle of oscillation was restored  to a constant 45°
to minimize coal packing in the drop sleeve.

    The improved charging procedures did  not solve the major
problem of maintaining an open gas passage at the top of the oven.

    Additional data is shown on Table  3 for  five charges made
in December, 1973 with coal having a typical 7% moisture utiliz-
ing automatic leveling with P-4 pusher.   This represents the best
results that can be expected with this charging system.

OVEN PRESSURE DURING CHARGING

    This charging system has not achieved low oven pressure dur-
ing the entire charging cycle.  On an oven with good aspiration
and with consistent coal flow from all three hoppers,  the pressure
at the smoke hole (coke side of the  oven) when measured has
typically averaged  -1" to +1" w.c. from the  start of the charge
through the initial period after leveling starts.   Approximately
5-8 seconds after the final feed starts,  the oven pressure at the
smoke hole typically increases to +8 or +10" w. c .   As soon as
the coal feed is complete and the butterfly  valves are closed,
the oven pressure decreases.  The period  of  unacceptable emissions
corresponds to the time representing the  final 20% coal feed dur-
ing which time leveling occurs.  The increase in pressure at the
coke side smoke hole verifies the constriction of thegas passage
at the top of the oven.  Details on  pressure measurements are
given in Appendix A, complete with a  pressure recording.

    The average performance can be somewhat  improved by initiat-
ing leveling at the start of the charge.  This improvement is
the apparent effect of distributing  the coal charge more uniformly
in the oven so that an increased gas passage space exists at the
top of the oven for a given amount of  coal charged.  Although this
method will typically reduce emissions, it still does not produce
a smokeless charge.   It has one serious drawback.   If the coal does
not start flowing from all hoppers at  the start of the charge,
the leveling time will be excessive.   The excessive exposure of

                               75

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OVEN PRESSURE DURING CHARGING (continued)

the leveler bar in the oven can result in it being overheated.
Consequently this method is not recommended as a production
procedure with the present leveler bar.

ANALYSIS OF THE PROBLEM

    The reason why it is not possible to get consistent smokeless
charges can best be understood by a review of the method for
assuring an open gas passage during charging.  To maintain an
open passage, it is necessary that the coal charged in any given
port does not back up inside the charging hole sufficiently to
form a block.  The chances of doing this are minimized if the
coal to be leveled is shared at all three charging holes.  Prior
to leveling, the coal should be poured at proportional feed rates
that will result in uniform peaks near the coal level line (Figure
30).

    At this time about 76% of the charge is in the oven.  As coal
feed resumes the leveler bar will distribute the coal.  When
approximately 91% of the coal is in the oven and leveled, the
flat tops will extend about one foot past the charging hole flare
opening.  At this time the approximate remaining average coal
charge per hopper is 21 ft3 including all coal in the charging
hole flares and the leveler bar.  As a consequence the gas passage
is constricted and internal pressure starts to build-up.  It is
desirable that this portion of the charge be completed as soon
as possible to minimize emissions.

    With optimum coal flow conditions, there will probably be
some emissions associated with the last half of the leveling cycle,
The quantity of emissions will be influenced by the required
leveling time and the quantity of roof and flare carbon within the
oven.

    The smokeless charges that have occurred are generally the
result of slight undercharging,  uniform coal feed, minimal roof
and flare carbon, and adequate suction.

    If the coal feed pattern from the three hoppers is not
relatively uniform, excessive leveling will be required at one

                               76

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OVErtt  COAL,  PROFILE DURIKG!
          7G% COAL CHARQE PRIOR To
           COAL.
                             BO

-------
ANALYSIS OF THE PROBLEM (continued)

charging hole (the one with the slow feed).  This increases the
leveling time during which the gas passage is constricted.  It
also increases the length of the constricted gas passage.

SUMMARY OP RESULTS

    This test program has demonstrated that with all components
functioning as designed the emissions cannot all be directed into
the gas collecting main on a consistent basis, under the following
conditions:

1.  Using the maximum acceptable amount of oven suction as generat-
    ed by the aspirating steam system.

2.  A single gas outlet from the oven to the gas collecting main.

3.  With gas flow constrictions resulting  from coal flow and the
    presence of the leveler bar in the oven during the final coal
    charge.

The experience of charging with this coal  feed system indicates
that the relative feed rates among the three hoppers cannot be
controlled consistently to minimize leveling.  Refer to the emission
data sheets for December in Appendix D.  A procedure is necessary
that does not require consistent coal feed rates to minimize
constriction of the gas flow within an oven.

SOLUTION

    To approach consistent smokeless charging conditions, it is
necessary that this system be modified by  the addition of a
second gas off-take at each oven.  A double gas off-take provides
the means for assuring, an open gas passage at the top of the oven.

    J&L has investigated methods for reducing emissions on other
batteries at the Pittsburgh Works.  This included the installation
of "jumper pipes" connecting the smoke hole ports of adjacent
ovens.  The smoke hole can be seen in Figure 5.  It is located on
the coke side of the oven and has the appearance of an outlet to
a second collecting main.   The addition of the jumper pipe

                                78

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SOLUTION (continued)

provides a second gas off-take from  the  oven,  by permitting gases
from the oven being charged to reach the gas  collecting main
through an adjacent oven  (Figure 31).  During charging, in
addition to the normal procedures  in placing  the oven "on-the-
main", the jumper pipe is opened and the aspirating steam is also
turned on at the adjacent oven.  Since this adjacent oven is well
into the coking cycle, it can handle the charging gases from the
coke side of the oven in addition  to its own  coking gases.

    Two such jumper pipes were recently  installed on oven 1-1
and 1-2 on P-4 battery.  The arrangement of these jumper pipes
can be seen in Figure 32.  Charges made  on these ovens have
resulted in emissions that exceed smokeless charging conditions foran
average of 8.4 seconds.  The average results  of 15 charges are
shown in Table 2 (pg.6).  The data for 10 of  those charges are
part of Appendix D.

    It is apparent from the data that the cycle time of charges
with jumper pipes equaled or bettered the fastest charging times
obtained with a single gas off-take.  The actual time for the
coal feed increased slightly.  This  was  the result primarily
with experimenting with different  coal feed sequences.  The
charging results have not been significantly  affected by the
different coal feed procedures.  Consequently it is believed that
emptying the hoppers simultaneously  will result in emissions
that will equal the average shown on Table 2.   With this method
of coal feed a charging time of about 2.4 minutes can be realized
with normal coal flow.

    The charge cycle time is decreased because the charging holes
can be sequentially relidded smokelessly without waiting for the
leveler door to be closed.

    As a result of test work on the  single gas off-take system,
and observations using the double gas off-take ("jumper pipes"),
it is recommended that a double gas  off-take  be used to provide
the adequate control of oven pressure necessary to ensure the
success of this concept.

    The required elements of this charging system to adequately


                              78 a

-------
SOLUTION (continued)

control oven pressure are as follows:

1.  Double gas off-take
2.  Adequate steam aspirating system
3.  Sealed oven ports
4.  Controlled coal feed system
5.  Sequential relidding of oven ports

THE EFFECT OF PROCESS VARIABLES ON EMISSIONS

Steam Pressure and Temperature

    The relation of steam pressure to emissions during charging
                               79

-------
                   \JuMPE/Rr  PlPElr  CHARGING?
oo
O
                                                                    PIPE
                                                            To ADJAC&MT
                                      Figure 31
                                                             OfF' -

-------
                               PIPE,
                                                    &L&OJAT
                                                    COV&Rr
                                                    HlMCfE
VAL.VJS
                                                      X
                                                        OI/E.M
                                             32

-------
Steam Pressure and Temperature (continued)

was difficult to determine on normal charging of ovens with a
single gas off-take.  This is demonstrated  by the results shown
on Table 5 which are discussed on page 70.   The previous discussion
has indicated how the constriction of the gas passage during
leveling was the major factor in determining the quantity of
emissions.  Increased emissions can normally be observed when the
header steam pressure is less than 120 psi.

    The increased aspiration results in more coal carry-over
into the gas collecting main.  Prior to the  installation of the
new larry car some rough measurements were  made using a temporary
high pressure steam line and compared to that existing at the lower
steam pressure level.  The greater aspiration was the result of
increasing the steam nozzle from 1/2" to 3/4",  increasing the
steam header pressure from 100 psi to 175 psi,  and increasing
the diameter of branch piping from 3/4" to  1 1/4".  The method
used to measure the coal carry-over is outlined in Appendix G.
The results of all testing  indicate that the  carry-over during
charging increased by a factor somewhere between 3:1 and 6:1.

    The results  (Appendix G) of collecting  ammonia liquor samples
from the gas collecting main just downstream verifies an increase
in coal carry-over with the new larry car.

Coal Analysis and Moisture Content

    The analytical properties of the coal had no apparent signifi-
cance on the quantity of emissions during charging.   The constrict-
ion of the gas passage during leveling made  it difficult to
determine the extent to which coal analysis  contributes to charg-
ing emissions.

    The moisture content of the coal did have an affect on the
quantity of emissions.  The results of 10 charges made in
January 1974 with coal having 8.3% moisture  can be compared with
the normal results obtained from five charges in December 1973
using P-4 pusher in which the coal moisture  was 7.1%   The wet
coal prevented uniform coal flow.  Only 40%  of the charges had
normal charging times.  The operator used a  bar on at least one
drop sleeve to get the coal flow started on  six of the ten

                               82

-------
Coal Analysis and Moisture Content (continued)

charges.   The average charging time increased 30% and T3
emissions increased 40 %.  At the same time T2 emissions decreased
45%.  The overall increase in emissions is attributed to longer
required  leveling time as a result of irregular coal feed.

Effectiveness of Oven Port Seals

    A poor leveler door seal will cause increased emissions from
the charging hole ports as well as the leveler door during the
final 20% charge.  It also causes emissions during the first
portion of the charge.

    Poor  seating of the feed hopper drop sleeves will leave an
open gap  in part of the charging hole ring.  During the last 20%
of the charge, the positive oven pressure produces flames which
damage larry car equipment.

Type and  Condition of Ascension Pipe

    There are two types of goosenecks used on this battery.  Their
characteristics are described in the section on Charging Equipment
Description,  (page 59).  The gas flow characteristics from the two
different designs tends to be,about the same, since the
conventional gooseneck has a larger steam nozzle.

    The conditions of the standpipe, gooseneck, and steam nozzle
limit the performance of the gas aspirating system.  The steam
nozzle must be clean and free of carbon deposits that constrict
the path  of the steam jet in the gooseneck.  The ascension pipe
must remain relatively free of carbon deposits.  Constrictions
near the  top of the standpipe limit the suction more than those
at the bottom.  Less than 80% opening at the top or 50% at the
bottom will usually result in a visible increase in emissions.

    Similar changes are noticed when the gooseneck or return bend
opening is less than 80%.

    The standpipe cap must have a good seal to assure good steam
aspiration.  Any air drawn in at this source will reduce the
oven gas  flow through the standpipe.

                               83

-------
Coal Charging Time and Charge Cycle Time

    The coal charging time starts when the butterflies first open
and oscillate.  It ends when the last butterfly  valve closes
the final time.  This time is directly related to  the coal  feed.
In general the shorter times occur when uniform  feed conditions
exist on all three hoppers.  Coal moisture will  cause the charg-
ing times to increase, but if the rate of feed remains uniform
in the three hoppers, this increased time will usually not  result
in more emissions.  If the increased time is  caused  by non-
uniform feed conditions between hoppers, then emissions are
expected to increase.  This is the result of  increased leveling
time during which severe gas passage constrictions cause
increased oven pressure.

    The charge cycle time includes the time required for closing
all oven ports in addition to the charging time.   The charge
cycle time starts at the same time as the charging time and ends
after all oven ports have been closed.  With  good  charging  condi-
tions, the emissions in re-lidding are not significant.  The
emissions that normally occur in the last 20% coal feed are
reduced as soon as all butterfly valves are closed.   If
significant emissions occur at the end of a charge,  they are
apt to continue while the leveler door is being  closed.  Once
the leveler door is closed re-lidding of charging  holes is
usually performed without significant emissions, except for
conditions of very poor oven suction or a constricted gas
passage resulting from insufficient leveling.

    Removing the leveler bar and closing the  leveler door takes
about 50 seconds.  Sequential re-lidding of charging holes  (1-2-
3) takes 12 seconds each for the first two and about 18 seconds
for the final one.  The first two re-lidding  operations require
12 seconds to replace the lids and start oscillating.  The  next
re-lid sequence can be initiated at this time.   The  final re-lid
sequence requires the lid lifter cycle to be  complete before
moving the car.

Weather Conditions

    The weather conditions have little direct relation to the
                              84

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 Weather  Conditions(continued^

charging  performance with respect to emissions.  To the extent
that it affects the  coal moisture,  it is a determining factor.

    There have been  additional  problems when the larry car is
first placed in service during  wet weather.  The wet hoppers
and drop  sleeves cause irregular coal feed for the initial two
or three  charges.

    The visual determination of charging emissions is influenced
by background light  and wind velocity.

System Malfunctions

    Any failure with charging equipment that adversely affects
the oven  port seals,  coal feed, maintenance of open oven gas
passage,  oven suction or proper re-lidding will tend to increase
emissions.  Good consistent charging requires reliable operation
of equipment.
                                85

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                            SECTION VII

                  PROJECT RESULTS - PROCESS CONTROL

 COKE PRODUCTION

     The charging system is designed to perform  consistently with-
 out any reduction in coke production rates.  The  general  criteria
 are to satisfy a pushing schedule of 60 ovens over an eight hour
 period.  P-4 Battery has a maximum pushing capability of  40 ovens
 during an eight hour production turn.  This  is  an average total
 charging cycle time of 12 minutes.

     The following charging time log is typical  of the results
 expected with the following conditions:

 1.  Single gas off-take.

 2.  Poking of coal with a steel rod not required  to start and/or
     maintain coal flow.

 3.  Subsystems perform reliably with no malfunction.

             EVENT                            ELAPSED  TIME (MIN.)

 1.  Start Charge (Oven 3-5)                  0
 2.  75% Charge Complete (#1,2,3)           1.0,1.1,1.1
     (Butterflies are Closed)
 3.  Start Leveling                           1.05
 4.  Open Butterflies (Final 25% Charge)      1.25
 5.  Hoppers Empty                            1.75,  1.95,  2.1
 6.  Request leveler Bar removed and Leveler
     Door Close                               2.6
 7.  Leveler Door Closed and Sequential Relid
     Starts            '                       3.7
 8.  Re-Lid Complete                          4.55
 9.  Complete Damper Off at Oven 3-9 and Re-
     move Lids at Oven 3-7                    5.55
10.  Get Coal at Bin and Move to Oven 1-7
     (Typical Average)                        8.05
11.  Manually Clean Gooseneck (1-7) and put
     Oven 1-7 on-the-main.                    9.55

                                86

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COKE PRODUCTION (continued)

These indicated total charging cycle times will not be attained
if the coal does not flow properly from all hoppers. Poking of
coal in the drop sleeve with a steel rod can result in an
increased charging cycle time of one to three minutes.  This
problem,  resulting from wet coal conditions, does not occur on
every charge.

    Typical times for such a case are as follows:

        Event	       Elapsed Time (Min.)
1.
2.
3.
4.
5.
6.
Start Charge
75% Charge complete (#1, 2, 3)
Start leveling
Open butterflies (final 25%)
Hoppers empty (1, 2, 3)
Balance of event times normal
0
1.0, 1.0,
1.05
2.0
2.3, 2.3,
11.05

1.85


3.6

For this charge the coal did not start out of #3 hopper immediately
and required the use of a coal poker.  Apparently more of the coal
from #2 hopper went to the coke side of the oven.  Consequently
considerable leveling was required to permit coal to discharge
from #3 hopper.  The coal actually backed up into #3 charging
hole until removed by the leveler bar.

    With a normal operating battery there are anticipated delays
that must be incorporated in any over-all production schedule.
Delays which affect pushing also affect the charging schedule, since
the pusher machine may not be available when required for charging.
These delays can be associated with equipment malfunctions, system
problems (coke difficult to push from oven),or personnel breaks
(eating lunch).

    When equipment malfunctions occur, it may be quicker to repair
the machine, rather than place a spare in service.  At P-4 battery,
it takes about twenty minutes to change the drop sleeve mounting
position when transferring operation of the P-3 larry car from P-3
to P-4 battery or vice-versa.
                             87

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COKE PRODUCTION (continued)

    A normal pushing schedule would  anticipate delays of about 10%
of the total operating time.  An  eight  hour turn would achieve full
production with about 48 minutes  delay  from all sources.

    It is evident from the total  charging cycle times indicated
that the larry car can satisfy the schedule of 40 ovens per turn
at P-4 battery.  Recognizing 10%  delays,  the required total cycle
time is 10.8 minutes or less.  This  compares well with the 3.55
typical total cycle time.

    It is evident that this system as described for a single gas
off-take system would not meet the requirements of an eight-hour
pushing schedule of 60 ovens.  Again recognizing 10% delays,  the
required total cycle time is 7.2  minutes  or less.   Since a
double gas off-take is required to achieve an acceptable level
of smokeless charging, the cycle  time will be evaluated under these
conditions.  It must be recognized that the optimum changing procedure
may not be determined until "jumper  pipes" have been installed on
the entire battery.  Using the times required for re-lidding (does
not wait for the leveler door to  close) the following charging time
log should be typical of good operating conditions.  Events 6 and
7 are now performed in parallel and  independent of the charging
sequences.

5.
8.
9.
10.

11.

Event
Hoppers empty
Re- lid complete
Complete damper-off
Get coal at bin and return to
next oven
Manually clean gooseneck and put
oven on-the-main
Elapsed
1.75, 2.4,
3.2
4.2
6.7

8.2

Time
2.0






    This total cycle time of 8.2 minutes  will  not satisfy the 60
oven pushing schedule where the corresponding  time of 7.2 minutes
or less is required.  The problem  in  satisfying this schedule
is not directly related to the actual  charging sequence (3.2
minutes) ,  but rather to the additional procedures involving "damper-
ing off" and "cleaning goosenecks".   If the  lidman was used to
                                88

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COKE PRODUCTION (continued)

"damper-off" (oven to be pushed) and  "remove lids"  (oven  just
pushed), the cycle time would be 7.2  minutes.  An additional minute
could be saved if the larryman cleans the gooseneck of  the  oven  just
pushed during charging.  With either  of these modifications to the
system, a total cycle time of 7.2 minutes would be achieved
permitting an eight-hour pushing schedule of 60 ovens.

BY-PRODUCTS

    Directing all the charging gases  into the collecting  main
by using greater oven suction may affect the by-products  as
result of
1.  Increased gas in the system
2.  Increase in coal carry-over
3.  Increase in oxygen level
4.  Increase of NOX

    The coke oven gas and tar were measured to determine  the
existance of any adverse changes in quality.  One of the  problems
associated with oxides of nitrogen is the formation of  gummy
substances.  The gum content of the circulating wash oil  was
monitored.

    The by-product system receives the raw gas from five  batteries,
and the influence of P-4 battery on any changes to the  system can-
not be directly determined.  "Jumper  pipes" have been installed  on
the other four batteries to direct the charging emissions into the
collecting main.  Several tar samples were taken at #9  and  #10
crossover, to monitor the tar from P-4 battery prior to reaching
the decanter tanks.

TAR

    Any increase in coal carry-over would be expected to  show up
in the tar processing system.  The job of the "Tar-chaser"  is to
clean out the sludge from the gas collecting mains on a weekly
basis.  He has observed no change in  the sludge taken from  the
collecting main at P-4 battery during the past year.

    The sludge taken from the flushing-liquor decanter  tank is
reported to have increased about 15%  during the past year.  The

                                89

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TAR (continued)

pitch sludge buggies from each of  five  decanter tanks are emptied
on a daily basis.  During the past year the average sludge leve
in the buggies has increased about 2" - 3".   This may also be
partly the result of new conditions on  the  other four batteries.

    Tests were performed at the P-4 battery cross-over to determine
the effect of steam pressure on the amount  of coal carry-over  in
the tar.  Tar samples were collected for  a  20-hour period with
the aspirating steam pressure set  at 130  psi.   The samples were
taken at a point at #9 cross-over  just  before it gets to the flush-
ing-liquor decanter tank.  Eight hour tar samples were then taken
at 180 psi.  The results are shown on table 6.   The tar samples
were examined under a microscope to determine the type and size
of particles.  The results (refer  to Appendix G)  show that the
particles of coal, semi-coke, coke, and pyrolytic carbon (similar
to wall and roof carbon) increased in quantity and particle size.
The steam pressure is normally set at 130 psi - 140 psi at the
header.  The quinoline insolubles  at 130  psi were about 20%
greater than the 1968 average (100 psi  aspirating steam pressure).

    There has been no significant  change  in  the by-product tar
as measured at the tar pump after  the ammonia liquor decanter
tanks.  The test results in Table  7 show  no  significant change
from the 1968 average tar or the tests  made  in August 1972 just
piror to the operation of the new  charging  system,  and prior to
the installation of jumper pipes on the other batteries.
                                90

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             Table 6.  TAR SAMPLES P-4 BATTERY




           (#9 Cross-over just ahead of decanter)
Measured Parameter
Steam pressure (psi)
Qu incline insoluble (% wt.)
Benzene Insoluble (%wt.)
Ash (% wt.)
Coal Properties _
Bulk Density (lb/ftj)
% Volatile Matter
% Moisture
% Fixed Carbon
% Ash
Oil pts./ton coal
Pulverization
% on 3/4"
% on 1/2"
% on 1/4"
% on 1/8"
% through 1/8"
% through 100 mesh
20 Hr.
Sample
2/23/74
130
8.9
12.7
0.14

43.1
32.25
8.01
60.65
7.10
2.8

0
1.1
5.6
16.0
77.3
10.6
8 Hr.
Sample
2/27/74
180
11.5*
18.0
0.32

42.80
32.27
8.51
60.50
7.23
2.8

0
1.6
4.4
16.3
77.7
10.6
Coal evident in Quinoline Insolubles from this sample (180 psi)
                           90 a

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          Table 7.  PRODUCTION TAR ANALYSIS

              (Sampled after decanter)
Measured Parameter
Specific gravity at
15.5°C
Engler viscosity at
140°C (sec.)
NH4C1 (lbs/1000 gal)
H20 (% vol.)
Distillate to 250°C
(% wt,% vol.)
Quinoline insoluble
(% wt . )
Benzene insoluble
% wt
Ash (% wt.)
Analysis-Dry tar
basis
Tar Acids (% wt. ,
% voL)
Tar bases (% wt. ,
% vol.)
Napthalene (% wt.,
% vol.)
Creosote (% wt. ,
% vol.)
Date
1968
Avg. '.
1.216
—
2.0
3.2
b
UJ9^U
7.1
10.5
--

1.3/L5
0.6/0.7
6.3/7.6
4.2/5.0
1972a
J/28-9A •
1.203
840
2.4
5.0
B.345.6
7.6
11.3
0.047

1.5/L.7
0.7/0.8
7.5/6.9
4.3/5.0
1972
lQ47-]0/28 !
1.204
680.1
1.7
3.8
14.647.4
6.9
10.3
0.013

1.VX4
0.7/0.8
8.64D.3
4.9/5.7
1973
H-J45
1.203
833.1
3.1
5.8
B. 846.4
7.7
11.7
0.04

0.9/L.2
0.6A7
8.5/10.0
4.4/5.2
1973
5&-5&
1.210
795
5.8
2.5
15.7/18.7
6.7
10.2
0.06

0.9/U
0.6/).7
9.6/LM
5.6/6.2
1973
12/21-J2/31
1.203
680
3.6
4.5
14^17^
8.0
11.0
0.045

L2A3
0.6A7
9^/4.9
4.^4.9
a.  Sampling performed just prior to start of new system
b.  11.8/14.1 is per cent by weight, then volume
                         91

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COKE OVEN GAS

    The quality of the coke oven gas (Table 8) has shown no
significant change during the past year.  The air content of the
gas has increased (23-25%) as evidenced by an increase in nitrogen.
This has probably contributed to a slight decrease in the BTU
value of the gas.

    The oxygen content of the coke oven gas from all five
batteries has not shown any significant change during the past
year.

    Some oxygen sampling was performed on P-4 battery raw gas at
each of two gas cross-over mains  (#9 and #10).  There were several
samples in which the oxygen content exceeded 2%, with a maximum
reading of 3%.  The average value measured at the two cross-overs
was slightly over 1.2%.

    It should be noted in snap sampling that the oxygen content of
the gas depends on local events on the battery that influenced a
particular volume of gas.   A second sample taken moments later
could result in a dramatic change of oxygen content.  The conclus-
ions from all oxygen sampling are that the system has had no
significant affect on the oxygen content of the coke oven gas at
#9 and #10 crossovers.  It must be recognized that the sampling
was related to single gas off-take oven conditions, and that the
addition of "jumper pipes" could alter the results.

    The presence of increased oxides of nitrogen is not evident
from tests made of the gum content of the circulating wash oil
shown in Table 9.

    The gas at #9 and #10 cross-overs was also sampled for oxides
of nitrogen using the A.S.T.M. D-1607-60 method.  No oxides of
nitrogen could be detected using this method of analysis and the
laboratory sampling techniques.

COKE OVEN GAS VOLUME

    The decrease in emissions is expected to result in an increase
in the average volume of coke oven gas.  Measurements made in the
standpipes during charging (Appendix G) indicate approximately
1135 CFM additional gas was drawn with high pressure steam ejection,
                                 92

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             Table 8.  COKE OVEN GAS ANALYSIS
Measured Parameter
CO2 (% vol.)
Illuminantsc (% vol.)
02 (% vol.)
CO (% vol.)
H2 (% vol.)
CH4 (% vol . )
N2 (% vol.)
BTU (Gross)
BTU (Net)
Spec, gravity
H2S in gas (grains/
100 ft3)
HCN in gas (grains/
100 ft3)
Date
1970
Avg.
2.9
3.0
1.3
6.6
49.2
32.4
4.9
551
501
'0.41
300
54
1972a
835-9A
2.5
3.0
1.5
6.3
49.9
31.1
5.8
542
492
0.41 '
322
193
1972
X/L7-1&8
2.3
3.0
1.3
6.2
49.9
30.3
7.0
535
486
0.41 '
328
42

1973
3/M/L5
2.2
2.9
1.2
6.3
49.8
30.5
7.0
535
485
0.41
195
50
1973
5/14-5/31
2.4
3.0
1.3
6.3
49.8
29.9
7.3
531
482
0.41 •
280
32

1973
Dec.
3.0
2.8
1.3
6.4
49.5
29.6
7.4
524
475
0.42
—
—
a.  Sampling performed just prior to start of new  system
b.  Includes any acidic gases such as H2S, HCN, etc.
c.  Any constituents that will react with fuming sulfuric
    acid; mostly unsaturated hydrocarbons such as  ethylene-
    C2H4
                           93

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Table 9.  GUM CONTENT OF CIRCULATING WASH OIL


Measured Parameter
Insoluble gums (g/1.)
Soluble gums (g/1.)
Total gums (g/1.)
Date
1972
8/24
0.34
0.12
0.46
1972
10/27
0.14
0.18
0.32
1973
1/12
0.28
0.31
0.59
1973
5/18
0.31
0.13
0.44
1973
6/1
0.25
0.14
0.39
1973
Dec.
0.18
0.18
0.36
                     94

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COKE OVEN GAS VOLUME  (continued)

when compared to the  original  low pressure steam.  Extropolating
those results for the present  header pressure of 130-140 psi,
indicates an approximate  increase of 50% or about 570 CFM additional
gas.  Assuming an average  steam aspirating time of 4.5 minutes, and
five charges per hour, approximately 12/800 ft3 additional coke
oven gas is produced  per hour.   Approximately 800,000 ft3/hr.  of
coke oven gas is produced  at P-4 battery.   This represents a
calculated increase of 1.6% The addition of jumper pipes to this
battery could result  in an additional 75% increase or about 9,600
ft3.  The overall increase in  coke oven gas of about 22,400 ft3
represents a 2.8%increase  with jumper pipes over the original
production.  This increase represents the emissions that formerly
went into the atmosphere as well as an increase in the quantity of
air drawn -into the system.

    The importance in minimizing the time span during which steam
aspiration is used, can be related to the operation of the primary
cooler.  During the summer an  excessive increase in gas will overload
the primary cooler causing an  increase in the gas temperature.
If the limits of the  gas exhauster are reached,  the increased  back
pressure will reduce  oven  suction.

    The recording charts for coke oven gas show significantly  higher
peaks than previously.  These  peaks are attributed to excessive use
of steam on ovens not being charged.   These charts also indicate
that approximately 100,000 ft  /hr.  more coke oven gas is now
produced from the five batteries,  over that produced 18 months
earlier.
                               95

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                           SECTION VIII

             PROJECT RESULTS - EQUIPMENT PERFORMANCE

GRAVITY FEED LARRY CAR

    As part of previous development work, a full scale gravity
feed hopper had been built and tested at the Swissvale yard of
Koppers Company (Figure 33).  The purpose of that test was to
en-sure that the basic C9ncepts of the feed system could be
realised prior to building the new larry car.  Some of the
conclusions in the test report indicated that:

1.  The hopper and butterfly valve can control the flow of all
    type coals to maintain a coal seal in the hopper at all times.

2.  The system provides for nominal misalignment problems.

3.  The hopper can satisfactorily discharge coals having a wide
    range of moistures (4-9% on final test)

4.  The system provides a uniform coal flow rate during the
    entire emptying interval.

    The experience to date indicates that these conditions
were only partially achieved in full production operations.

Maintain Coal Seal

    The flow of coal from the hopper and drop sleeve is such
that a coal seal is maintained continually.  At the end of
charging, as sensed by a bottom coal level detector, the butterfly
valve is closed so that a 15" layer of coal seals the charging
hole.

Drop Sleeve Misalignment

    The design of the drop sleevewas such that with an initial
misalignment of 1 1/2", the sleeve was to seat within the charg-
ing hole ring.

    In order to satisfy the alignment tolerance conditions, the
charging hole rings were realigned by freeing them from the

                               96

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               HOPPER -
               OJAZER
               S&CTIOU
   33
97

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Drop Sleeve Misalignment (continued)

permanent brick and re-positioning so they were concentrically
aligned with the drop sleeves.  The surface in the  immediate
vicinity of the rings was leveled so as not to interfere with the
housings for the butterfly proximity limits and the hydraulic
driven rotary actuator.

    The alignment of #3 charging hole rings could not be optimized
in many instances because to do so would result in a constriction
of the charging hole under the ring and would result in exposure
of part of ring to the oven gases.  The net result  is that many
of these rings are slightly displaced to the coke side with
respect to the drop sleeve by approximately 1/2" to 1".

    The original seating performance was unsatisfactory.  The
rotary actuator housing or limit housing would strike the battery
surface because of a swing motion of the drop sleeve.  This
would prevent the drop sleeve spherical surface from properly
seating in the charging hole ring.  A new spherical ring was made
with a 1/2" extension.  This permitted the drop sleeve to seat
without interference from the housings (Figure 34).

    The drop sleeves used to swing as they were lowered.  This
was caused principally by the drop sleeves not being balanced
and the downward motion tends to be in an arc that  is restrained
by vertical guides.  Also the connecting link between the lowering
arms and the drop sleeve pin was solid.  If the drop sleeve seat
made contact against the charging hole ring in such a manner that
it was tilted, it could be driven against the ring.  Instead of
permitting the sleeve to slide in, it would jam it against the
side of the ring.  Three modifications were made to correct the
problem.  The drop sleeves were counter-balanced with weights.
A slotted link replaced the solid link.  A guide was also furnish-
ed to force the drop sleeve to be directed downward without
significant oscillation.  These modifications for the most part
corrected the seating problem.

    The pins and links which are part of this system must be
maintained free with frequent lubrication,  to allow proper seat-
ing.
                                98

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                       DROP SLEEVE SEATING
THE DROP SLEEVE SEATED IN CHARGING HOLE RING WITH EXTENDED SPHERICAL
SEATING RING.  NOTICE A COUNTERWEIGHT BOLTED TO FRONT OF BUTTERFLY
LIMIT HOUSING. THIS WEIGHT HAS SINCE BEEN REMOVED. A SOLID LINK CAN BE
SEEN BETWEEN THE LOWERING ARMS AND THE DROP SLEEVE PIN.  THIS WAS
CHANGED TO A SLOTTED LINK.
                            FIGURE 34
                                99

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Drop Sleeve Misalignment (continued)

    At the present time #1 and #2 drop sleeves seat consistently
in the charging hole rings.  There are still occasional problems
with #3 drop sleeve seating.  This problem exists because the
charging hole rings on some ovens cannot be moved sufficiently
to provide optimum alignment with the drop sleeve.  The seating
problem could be improved by moving #3 hopper  (coke side) to
provide a better average position.  This would be a major job.

    For a new installation where hopper and drop sleeve alignment
are optimized, this system can provide for a limit of about 1 1/2"
misalignment, and still consistently seat properly.

High Moisture Coal

    The hopper can discharge coals over a wide range of moistures,
but the use of a vibrator is usually required.  The discharge
of the coal through the drop sleeve is more difficult, and the
presence of the vibrator on the hopper is not sufficient to cause
flow under all conditions.

    The use of vibrators, as originally installed, was a source
of problems since the car started operations.  The mechanical
vibration has caused many parts to fail because the fasteners
were loosened or sheared.  All such fasteners had to be welded
to prevent losing them.  During the interim period the sleeves
were dropped several times.  A drop sleeve return spring fractured
as a result of fatigue stresses.  The vibrators themselves failed
and it is believed that the failure mechanism was initially
mechanical wear in the bearing housing.  It caused the top level
sensors to loosen and drop the paddle wheel.  There were a few
times when it caused the hopper position proximity switch contacts
to vibrate if the drop sleeve was not fully down and the limit
was just on the verge o'f operating.  This would cause the butter-
fly valve to close for unexplained reasons.

    The worst symptom of this problem was discovered in July 1973
when fatigue cracks were found in the hopper body at the toe of
a circumferential fillet weld joining the type 304 stainless steel
hopper body to a carbon steel bottom flange.  This failure
occurred on all three hoppers.  Figure 35 shows the original
                               100

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                      HOPPER FATIGUE CRACK
NOTICE FATIGUE CRACK WHERE THE HOPPER BODY IS JOINED TO A BOTTOM
STEEL FLANGE.  THE VIBRATOR IS SEEN IN THE ORIGINAL MOUNTING LOCATION.
THE BOTTOM COAL LEVEL SENSOR CAN BE SEEN ABOVE. THIS HAS BEEN
REPLACED BY A COUNTERWEIGHTED ROD TYPE SENSOR.
                           FIGURE 35
                              101

-------
High Moisture Coal (continued)

vibrator mounting  position and an example of a  fatigue .crack.

    It was suggested that the vibrators be relocated on the
conical portion of the hoppers.  A solid base was prepared for
the vibrator which mounted on a long channel to  distribute the
vibration over a wide area.

    Since this change, there has been improved life with the
vibrators, and no evidence at this time of any mechanical
failures attributed to vibration.  However more  observation time
is required to make a definitive conclusion.

    Because of the drop sleeve design the coal  feed  is not reliable
when the coal moisture is approximately 8% or more. With  this moisture
content the operator must frequently use a steel rod to poke the hole from
the top of the drop sleeve in order to initiate  coal flow.  Once
the coal flow starts it will usually continue to pour.  The
emission data shown for charges made with 8.3% coal moisture in
January, 1974 indicate that the operator had to  use a bar on at
least one drop sleeve for six out of ten charges.

    The operator will try to get out of this troublesome problem
by oscillating the butterfly valves until the coal has been
completely discharged from the drop sleeves.  A  10-15" coal seal
will result in some packing of coal when the drop sleeve is raised
after a charge.   This small amount of packing causes no apparent
problem except with coal having a high moisture  content.

    The incidence of stalled butterflies during  leveling is
greatly increased during wet coal conditions as  described
previously in Section VI (Page 73).

Uniform Coal Flow

    Consistent coal flow from all three hoppers  would permit the
adjustment of coal feed rates to minimize the leveling time.
This feature was never achieved consistently.  The time charts
included with emission data (Appendix D)  for December 1973 and
January 1974 clearly indicate the variable feed  rates.
                                102

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 Uniform Coal Flow (continued)

     Some  of  the  problems affecting coal feed were discussed in
 the  previous paragraph on high moisture coal.  In addition two
 frequent  problems at the start of the project that resulted in
 coal packing were:

 1.   Too much coal left from the previous charge.

 2.   Drop  sleeves have to be raised for some reason after they
     have  been lowered,  but prior to charging.

     Even  with normal 1% moisture the coal would frequently pack
 after raising the drop sleeve,  if the coal seal was more "than 15".
 This condition seldom occurs since the installation of a bottom
 level sensor that maintains a  consistent 15" coal seal.  The
 second  problem occurs infrequently since the performance of drop
 sleeves in seating within the  charging hole rings has improved.

     Except for a few isolated  cases,  once the coal flow has
 been initially started,  it will continue,  though not necessarily
 at a constant feed rate.

 Improvement  of Coal  Flow Problem

     At  times with conditions of'high moisture,  the final coal
 seal appears to  be concave,  indicating a tendency for coal to
 pack around  the  sides of the drop sleeve.   The tapered insert
 between the  drop sleeve  shell  and the butterfly cylinder is
 believed  to  be a major  contributing factor.  The packing of coal
 at the  insert may cause  the  formation of a bridge above the
 butterfly.

     Several  steps were  taken to reduce the problem.   A coal poker
was  installed  in #3  hopper.  The  coal poker was hydraulically driven
 in a     vertical  cyclic  motion with its lowest point about 2"
 above the butterfly  valve.   The performance of this device was
marginal.  It  would  usually  work  when coal packed in Ihe drop
 sleeve because previously the  drop sleeve had been raised with
more  than a  15"  layer of  coal  remaining above the butterfly valve.
However with  very wet coal  (8% moisture) ,  it would frequently  fail
to break  the  bridge.
                                103

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 improvement of Coal Flow Problem  (continued)

    If the coal flow stopped because coal backed up  in the charg-
 ing hole, the use of the coal poker tended  to pack the coal and
 make the condition worse.  The coal poker was removed and a
 hydraulic vibrator was mounted directly to  the side  of #3 drop
 sleeve to see if this would improve the coal feed without damag-
 ing the charging hole rings.  The vibration force was adjustable
 by the setting of a hydraulic flow control  valve.  This device
 could be adjusted so that it would always start coal flow, but
 the vibrating force required was of a magnitude that would
 apparently result in eventual loosening of  the charging hole
 rings.  The environment of fire and vibration made it vulnerable
 to hydraulic hose leaks.  It has since been removed.

    A preferred solution is to re-design the hopper  drop sleeve
 so that the initiation of coal flow requires no auxiliary devices,
 The present drop sleeve insert has a 57° slope.  Work has been
 initiated into ways of achieving a minimum  67° bin angle, based
 on criteria which resulted from hopper design research by U.S.
 Steel.

 Minimize Stalling of Butterfly Valve

    When the coal backs up in the charging  hole ring, the buttei?-
 fly oscillation tends to pack the coal and  eventually stalls the
 butterfly.  The operator has been trained to watch the oscillate
 lights.  If they stop cycling ON and OFF, the operator resets the
 sequence alarm and waits 10-15 seconds.  This gives  the leveler
 bar time to remove enough coal to open the  charging  hole.  The
 operator can then start up the butterfly to complete the charge.
 This procedure appears to be effective at least 98%  of the time.

    An improved procedure would utilize coal flow meters to
 monitor the performance.  As soon as coal flow stopped as a
 result of coal backing up the charging hole, the butterfly
 oscillation could be terminated before it packs the  coal.

    A hydra ulic pressure gage was connected to the butterfly
oscillate hydraulic line.  The hydraulic pressure with no coal,
or with regular feeding of coal is the same.  Consequently the
operator cannot use this gage to determine  when coal is not flow-
 ing because it is packed above the butterfly valve.  When coal
                               104

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Minimize Stalling of Butterfly Valve   (continued)

 backs up  from within  a  charging hole/  the pressure goes up
 when the  butterfly  stalls,  and  this  is easily seen on a gage.
 It  does not  indicate  when coal  flow  stops,  but rather when the
 butterfly valve  stalls.   The  butterfly valve oscillate lights
 already provide  this  information,  consequently the pressure
 gage is of no use as  a  coal flow indicator.

Conclusions -  Coal Feed System.

     The present  coal  feed system has sufficient provision for
 normal misalignment with  charging holes,  and  is able to maintain
 an  adequate  coal seal at  all  times.

     The system does not properly discharge  coal with 8% moisture
 and must  be  redesigned  to achieve  this necessary goal.  The
 system does  not  provide a uniform  coal feed  during charging,
 but with  the addition of  jumper pipes,  this  feature is not
 required.  The control of the coal feed  is  necessary to ensure
 that leveling is required at only  one  charging hole.   The use
 of  coal level detectors can accomplish the  requirements,  if
 the coal  feed system  can  reliably  charge coal with 8-10% moisture.

     There are several desirable features which should be provided
 on a coal  feed system to  optimize  charging performance and car
 reliability.

 1.  The coal feed system  must reliably discharge coal under all
     normal operating  conditions (various amounts of moisture,
     etc.)  .

 2.  A sensor that can provide the  operator with coal flow
     information  from  each hopper is  desirable.

Hopper Volumetric Measuring  Sleeves

     The gravity  feed  hoppers have  been provided with adjustable
 measuring  sleeves.  These sleeves  are  very difficult to adjust
 and have  a tendency to come apart.   A  safety chain has been added
 to hold the  bottom section  of the  measuring  sleeve so that it
 cannot fall  into the  hopper.  The  measuring  sleeve sections were
 not balanced  and tended to  jam  together.
                               105

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Hopper Volumetric Measuring Sleeves (continued)

    The measuring sleeves have been re-designed to alleviate
these problems.   The modified design has not yet been installed.

Reliability Problems with Hopper Components

    The inability to be able to maintain negative oven pressure
during leveling  results in emissions during part of this opera-
tion.  This also affects the reliability of the car.  Internal
oven pressure causes flame to be directed out of the charging
hole between the charging hole ring and the drop sleeve,
resulting in damage to electrical sensors and hydraulic hoses.
This is particularly evident when the drop sleeve does not
seat properly in the charging hole ring, leaving an open gap
(almost restricted to #3 charging hole).

    The latest arrangement of hydraulic hoses and the latest
arrangement of proximity switches have reduced the possibility
of failure because of flame from the charging holes.

    The Original limit switches that monitored the hopper position
(UP, DOWN, CLEAR)  were hatchway type limits.  These had a very
short life since any heat from flame would cause them to fail
in spite of the  protective shielding.   The HOPPER CLEAR limit
is set to be actuated when the drop sleeve raises sufficiently
to clear the charging hole rings.  This permits the car to
travel by means  of operating the EMERGENCY TRAVEL PB.  These
limits were replaced by proximity switches rated 450° F, and
more elaborate heat shielding was added.  The performance of these
limits has been  reliable since that time.

    The original switches for the butterfly valve motion (CLOSED,
OPEN, CCW) were  and still are the proximity type switch.  The
switches are housed in a steel box which provides good protection
but is located very close to the charging hole ring and the
resulting source of flame.  The life of these switches has been
good at #1 and #2 butterfly valve.  The life of those at #3
butterfly has been considerably less because of the much more
frequent occurrence of flames from between the charging hole
ring and the drop sleeve.  There have been three butterfly
limits fail in 4 1/2 months, all at #3.

                              106

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Reliability Problems with Hopper Components  (continued)

    At the present time a high temperature material  rated 1800°P
is wrapped around the switches in order to prolong their life
(# 3 hopper).

    The wiring for these sensors has held up reasonably well.
It is rated for 1000° F temperature and is enclosed  in conduits
or armored cable.

    The maintenance of the butterfly valve hydraulic hoses has
been a problem.  The original hoseshad an extremely  short life.
Several different hoses were tried.  The best results were
obtained with a heat-resistant hose having a double  layer of
woven asbestos insulation under the armor.  The original hose
was an expensive 7 foot long piece that required removing the
rotatory actuator housing cover to change, a maintenance job
that normally took about 90 minutes.  The arrangement was
changed so that a 3 foot hose was required that takes about
20 minutes to change.

    The butterfly valve is powered by a rotary actuator.  Two
of these have failed during 16 months of operation.  The
mechanical failures were apparently associated with  slight
movement of the actuator housing during operation.   The mounting
design makes it difficult to anchor the housing in a manner that
prevents anymovement.

Hopper Coal Level Control

    At the beginning of the AISI program several coal level
sensors were tested on an existing Wilputte  larry car used on
P-4 battery.  These include a SONAR type device, capacitance
probe, pressure sensitive device, vibrating  rod, and a paddle
wheel drive device.  The results of this test work indicated
that the paddle wheel drive device was more  reliable then the
other tested units.  This particular unit was a  "Bin-0-Matic".
The second and third level sensor were applied with  a baffle
above the paddle to protect the unit when the hopper was being
loaded at the coal bin.

    After a year's use in production operation,  the  Bin-0-Matic
is still in use at the 80% level.  There have been only one or
two units changed in this position since the car was installed.
The units were changed because of an internal gear  failure.
                              107

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 Hopper Coal Level Control  (continued)

 The units are located in an area where  reliable  operation has
 been obtained and they are considered successful.

    The bottom level sensor did not prove adequate because  it
 was not located in a proper position to sense  the coal  level in
 the drop sleeve at which time the butterfly  is closed.   In
 order to maintain a proper coal seal of 15", it  is necessary to
 close the butterfly when the coal level just drops below the
 bottom of the hopper cylinder.  The Bin-0-Matic  was  located in
 the tapered part of the hopper, about 30" above  the  bottom of
 the cylinder.  It was mounted at this location,  since there was
 no mounting space available below that  point.  An electric
 operated timer was energized when the Bin-0-Matic was activated
 (no coal).   After a pre-set timed period, the butterfly  would
 close.  With a uniform coal flow this system would work.
 However the coal flow is quite variable in the final feed,and
 it was impossible to maintain a proper  coal seal.

    There were other problems associated with this bottom level
 sensor.  Being at the tapered portion of the hopper, the coal
 flow was not as regular.  The coal was  more apt  to pack  on the
 baffle creating an occasional void.  There was almost always a
 void that occurred just after the drop  sleeve was lowered.  This
 would cause the sensor to indicate "EMPTY" for about 5-10 seconds.
 This problem was eliminated by interlocking the circuit of the
 bottom level sensor so that the logic was available  only after
 the 75% level sensor was activated.

    The shaft of the Bin-O-Matic was more susceptible to coal
 packing,  apparently because of its location in the hopper.  It then
 is necessary for some one to climb inside the hopper and remove
 the coal from the shaft.  This might occur on the average of
 once a month.

    An attempt was made to use a Bin-0-Matic in  the  drop sleeve.
 This was rot successful since coal would pack around the shaft
 causing it  to stall,  thus indicating the presence of coal.  J&L
 then specified an arrangement for a bottom coal  level sensor
 consisting  of a counterweighted rod which extends into the hopper
where the original paddle wheel sensor  was located.  This

                              108

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Hopper Coal Level Control  (continued)

arrangement is shown on  Figure  36.   The absence of coal causes
the counterweight to rotate  the  rod  away from the hopper wall and
operate a proximity switch.   The presence of coal pushes the rod
to the cylinder wall, overcoming the -counterweight.  This device
has consistently maintained  a coal  seal in the drop sleeve and
has not yet required any maintenance.

    The Bin-O-Matic used at  the top of the hopper was subject
to failure from the hopper  vibration.   Also the top coal level
would drop frequently when  travelling  to an oven.  The operator
could not consistently use  this indicator to determine initial
coal flow.  The counterweighted rod was installed at the top of
the hopper and has been  working successfully in this location.

    On a new car the counterweighted rod type level sensor would
be recommended for all locations.   The length and position of the
rod can easily be adjusted  to be in the proper position to sense
coal flow and the coal level.  Its  moving part consisting of a
pivot pin is located outside the hopper away from the coal.   The
proximity switch sensor  is  also located away from the coal out-
side the hopper.

AUTOMATIC LID LIFTERS

    The lid lifters, as  originally  installed, were a source of
excessive maintenance which  resulted from two general problems:

1.  The close clearances between the magnet and the drop sleeves,
    and also the bottom  of  the  magnet  and a lid on the battery
    resulted in frequent mechanical failures.

2.  The environment  (Primarily  flame)  caused failures in elect-
    rical sensors and wiring, as well  as hydraulic hoses.

Close Clearances

    The problem of close clearances is unique with this installa-
tion.  The drop sleeve spherical seating ring had to be lowered
1/2" in the field to permit  the drop sleeves to seat, thus reduc-
ing the 2 1/4" design clearance, which never existed.  In addition

                              109

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//o PP&K.
                   Figure 36



                     110

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 Close  Clearances  (continued)

the drop sleeves do not always raise  the  full  amount  because of
the remaining coal load and friction.   If the  drop sleeve
raised within 3/4" of the top/ the hopper UP limit was  supposed
to indicate it in the UP position.  The clearance  is  further
reduced by the fact that the conduit  connection  for the magnet
wire and the contact lid limit can be  seen to  be higher than
the reference clearance point.  Thus with normal conditions the
clearance can be less than 3/4".  In  addition  to this,  at  times
the magnet assembly was tilted causing  the clearance  to be de-
creased.  Also the drop sleeve is not  always horizontal in the
UP position due primarily to an unbalanced remaining  coal  load,
particularly when excessive coal remained.

    The clearance between the bottom of the lid  lifter  magnet
and the top of the lid resting on the battery  was  even  tighter.
The approximate design clearance of about 4 1/2" did  not exist.
This clearance was based on a 1" flat  pancake  type lid.  The
type of lid used on this battery was originally  2  1/2"  with
lugs.  One quarter inch was later removed from the lugs reducing
the heighth to 2 1/4".  The lid lifter  did not always remain at
the elevation shown on the drawing.   Since a mechanical spring
arrangement is provided to raise the  lid  lifter  in case of an
electrical or hydraulic failure, a double-solenoid three-position
hydraulic valve is used.  Because of  internal  leakage,  the lid
lifter did not remain in the extreme UP position thus decreasing
further the clearances.

    On a 20 year old battery the surface  is not  uniform, thus
considerably reducing the apparent clearances.

    These close clearances at times resulted   in  interference
between the drop sleeve and the lid lifter.  The principal
problem here was damage to the conduit  boxes on  the magnet and
bent guide arms on the lid lifter mechanism.

    The close clearance between the lid lifter magnet and  the
lids on battery caused the lids to be  struck and moved  out of
position.  When the time came to replace  the lids  they  would
not seat properly.
                              Ill

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Close Clearances (continued)

    The following changes were made to minimize interference
problems:

1.  The hydraulic pressure was increased to 1300 psi to provide
    more force to raise the drop sleeves.

2.  The lever operated limit switch for HOPPER UP  sensing was
    subject to frequent failures causing the hopper to get an
    UP  indication when it was not sufficiently UP to have
    adequate clearance.  This was replaced by a more reliable
    proximity switch rated 450° F.

3.  The conduit boxes were revised so that the profile was
    decreased 1/4" to 1/2".

4.  The lid lifter guide arms were re-designed, with heavier
    steel  so they would not bend so easily.

5.  A wear bar is located between the lid lifter traverse wheels
    and the filler plate.  The last 18" of wear bar was removed
    to permit the lid lifter to lower 3/4" when it extends.
    The remaining wear bar was tapered near the end to provide
    a bumpless extend motion.

6.  The electrical circuit was revised to energize the UP
    solenoid at all times, so as to maintain the lid lifter in
    the full UP position to provide maximum lid clearance.

    There  were two other causes of interferences.   With the
hydraulic  pump shut off the two-position double solenoid valves
can be momentarily electrically energized or manually actuated.
The equipment does not move because there is no hydraulic
pressure.   When the pump is later turned on, the hydraulic power
will cause equipment to move in accordance with the present
solenoid position.   Thus it is possible to have a  drop sleeve
lower and  the lid lifter extend simultaneously when the car is
placed in  service after an extended outage.  This  is known
to have happened causing the guide arm to bend.

    This was corrected by initiating an EMERGENCY TRAVEL opera-
tion on all  parts of the car whenever the hydraulic pump start
                              112

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Close Clearances  (continued)

push button is operated, thus  causing  all  equipment to move to
the TRAVEL position.

    The other interference problem wa-s caused by excessive
amounts of coal in the battery where the  lids were placed.  This
would elevate the lids.  It  is believed that  instances have
occurred, when the lid was raised  and  tilted  because of coal,
that resulted in  jamming the lid between  the  mechanism and the
battery top when  the car passed over,  causing a failure some-
times manifest by a broken hydraulic cylinder rod.   This situa-
tion has been corrected by alerting the operating people to this
situation.

    Presently, this once serious interference problem is no
longer a significant factor, and the over  all car reliability
is much improved as a result.

Fire Damage

    During charging, if the gas passage way in the oven does
not remain open,  internal pressure causes  burning gas to blow
out of the oven between the drop sleeve and the charging hole
ring.  Since the opening is usually very  small it errupts with
a blow torch effect.  Although the lid lifter components are
for the most part about six feet from  the  center of the charg-
ing hole, they are occasionally subject to the heat of burning
gases.

    On a more frequent basis,  they are subject to heat damage
when lids are being removed from the oven  that was just pushed
(two ovens south of the one  just charged).  The heart of the lid
lifter parts are then located  directly over the oven that was
just charged.  If internal pressure exists in the oven,  flames
will be blowing out of the charging hole  between the circumference
of the lid and the charging hole ring. This  is very hard on
sensors and hydraulic hoses.

    The lever operated limit switches  cannot  stand up under this
abuse.  The contact blocks are destroyed  and  the mechanical
return springs are stress relieved.  In addition the wet

                               113

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Fire Damage (continued)

environment caused  by the presence of a quench tower results
in mechanical binding of the lever arm.

    There are six limit  switch sensors on each lid lifter.
EXTEND  and  RETRACT  limits monitor the horizontal motion, an UP
limit monitors  vertical  travel/  clockwise and counterclockwise
limits  sequence the oscillate motion, and a pin operated limit
indicates that  the  magnet has a  lid.  The first five sensors
were replaced at #3 lid  lifter with proximity switches rated
for 450° F  service.   These limits have greatly improved
reliability.  They  are still subject to temperatures which
significantly exceed the 450° F  for a short time.  These
switches are covered with a high temperature insulation  (Refrasil)
to protect  against  fire.

    The lever   operated limit which indicates that a lid is in
contact with the magnet  is still the original switch, simply
because it  is difficult  to use a proximity switch for this
application.  This  switch is used only for an operator's
indicating  light, and its failure will not interfere with the
control sequence.

    This switch is  also  well removed from the oven that was
just charged during a REMOVE LID operation on the oven that
was just pushed.  Consequently its exposure to heat is less
than the other  sensors.   There were two limit switch failures
in a year at this location.  About once every 4-6 months the
steel rod which protrudes from the magnet must be removed and
dirt cleaned out to prevent it from sticking.

    The clockwise and counterclockwise limits failed more than
any other sensor on the  lid lifters  (lever operated switch).
When these  fail the lids will not be oscillated when replaced,
but this will not stop the control cycle which allows so much
time to oscillate.   Consequently their failure does not
significantly affect the reliability since they do not stop
the process and can be repaired  or replaced when maintenance
people  are  available.  Failure to oscillate the lids will
usually result  in a  poorer oven  seal.
                              114

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Fire Damage  (continued)

    To  improve  the  electrical  reliability of the lid lifter
operation,  all  wiring  and  conduit work was re-routed in such
a manner  as to  minimize  exposure to flame and abrasive wear
during  operation  of the  lid  lifters.   One thousand degree
wiring  is used  on all  parts  of the lid lifter.

    There are two other  sensors associated with the lid lifters.
A current sensing device determines when the magnet is energized
or  de-energized.  This is  located in the control room as part
of  the  magnet control  and  has  not experienced any malfunction
to  date.

    The lid lifter  DOWN  sensor is a hydraulic pressure switch
located in the  hydraulic control cabinet.  This sensor has on
occasion  required a screwdriver adjustment to make it sense
when the  magnet is  lowered,  but has had no failures requiring
a replacement.  The adjustment is usually required, if at all,
when there is a significant  change in the temperature of the
ambient air.  An  adjustment  was required an average of two to
three times a year.

    The hydraulic hoses  which  operate the two cylinders are
also subject to failure  from exposure to burning gases.  These
hoses were replaced with a G-SM Goodall hose which significantly
improved  the life.

    The steps taken to minimize failures from damage occurring
as  a result of  exposure  to high temperatures have significantly
improved  the over-all  reliability.   There have been more failures
with #3 lid lifter  because it  is exposed more frequently to the
burning gases.  Since  September,  1973 there were three known
failures  with #3  lid lifter  caused by limit failures as a result
of  flame.   It is  believed  that the heat shielding will improve
this performance.

Magnets

    There have  been three  magnet failures since the car was
placed  in operation.   Two  were caused by lead wire exposure to
heat and  the third  was caused  by the  drop sleeve lowering into

                               115

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Magnets  (continued)

the magnet when  the  hydraulic pump was turned on  (this problem
has since been corrected).   This appears to be a  satisfactory
life span  (neglecting  the  third failure).  Part of this success
is attributed to the fact  that the magnet only holds the lid
while it is being removed  or replaced.  Thus the  lid temperature
is not a significant factor in magnet heating.

Hydraulic Panels

    The  arrangement  of hydraulic panels for each  lid lifter and
drop sleeve has  permitted  the operating people to get out of
trouble  in times of  failure, and has permitted maintenance
adjustments to be made more easily.

Improved Design

    Most of the  maintenance problems experienced with these lid
lifters  could be avoided on a new design.  Adequate clearances
could be assured in  the design.  The exposure of the lid lifter
to high  temperature  would  be minimal by locating the lid lifter
in the opposite  direction  so that when removing lids from the
oven just pushed,  the  lid  lifter is not directly above the oven
just charged.

    Careful selection  and  location of sensors and hydraulic
hoses will improve reliability.  The oscillate limits are not
required, since  this function can be performed hydraulically.
It is believed that  the present sensors (other than OSCILLATE),
properly applied and shielded will provide reliable service for
a re-located lid lifter, and will provide adequate service on
the present lid  lifter location.

DAMPER,  STEAM VALVE, AND STANDPIPE CAP OPERATING LINKAGES

    There have been  many problems with these linkage systems
and their performance  has  not been reliable.  With the present
operation, the larryman will always leave the cab to check the
operation.  If it was  not  properly executed, the lidman completes
the operation.
                              116

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DAMPER, STEAM VALVE, AND STANDPIPE  CAP  OPERATING LINKAGES
(continued)

    The major problems exist because  on an  old  battery (20  years)
the standpipes lean  in all directions and uniform dimensional
properties on each oven cannot be maintained.   The actuator
and linkage design did not incorporate  sufficient flexibility,
to account for this.  It was necessary  to increase the length
of the cross piece on the end of the  car operated rotary  levers
so that the operating band was increased from 1 1/2"  to 6".  A
guide plate was placed around the steam valve actuator magnet
attached to lever #2 so that the actuator shoe  plate  would
be properly held when the magnet was  not right  on center.   The
magnet power was increased by a factor  of four  to maintain
sufficient power to operate the linkage when not perfectly
aligned.  Further the linkages at each  standpipe had  to be  bent
to try to align for each particular set of  dimensional misalign-
ment.  In many cases extensions had to  be welded to the existing
levers.  #1 lever arm had to be extended 9".

Steam Linkage System

    In addition to the general misalignment problems,  the
following problems were experienced with the steam linkage
system.

1.  Steam linkage rods between the  shoe plate and the lever
    bend or break   (Figure 38) .

2.  The shoe plate binds to the pin and does not rotate freely.

3.  The linkage had to be counterbalanced to permit the steam
    to remain ON if lever #2 is lowered without energizing  the
    electromagnet.  This operation  is frequently required,  and
    can be performed with the EMERGENCY TRAVEL  PB.

4.  The linkage did not have sufficient means to adjust the steam
    valve so that it would turn fully ON and fully OFF each time.
    Frequently the necessary adjustment prevented the valve from
    being fully turned ON.

5.  Steam linkage levers had to be  bent to  provide adequate
    operation as a result of a leaning  standpipe.
                              117

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BENT STEAM LINKAGE ROD
       FIGURE 37
          118

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Steam Linkage System  (continued)

6.  On some ovens interferences exist between  the  steam valve
    linkages and the  lid operating  linkages  which  is  particularly
    noticeable when the oven  is dampered  OFF.   Figure 38 shows
    good clearance between the lid  operating mechanism and  the
    steam linkage.  Figure 39 shows a very tight clearance.

A new steam valve operating   linkage has  been  designed to
eliminate those problems.  It has not yet been installed.

Standpipe Cap Operating Mechanism

    The standpipe cap operating mechanism did  not  perform
reliably.  The following problems were  experienced.

1.  The original design had a lid rotate  shaft supported by a
    pillow block at one end and the gooseneck  lugs at the other
    side.  The pillow block was not designed for misalignment
    and was not particularly  suited for high temperature
    operation.  The shaft would bind in this pillow block
    preventing proper operation of  the  cap.   These pillow blocks
    were replaced with self-lubricating,  high  temperature,  self-
    aligning bearings rated for 1000° F service.  While this
    solved most of  the problems,  some additional shafts started
    sticking because  they were  larger than  the maximum allowed
    tolerance.  New shafts were made to replace the oversized
    ones.

2.  The shaft  lugs  on gooseneck frequently  broke because of the
    stresses  that  occurred when the cap reached the open limit.
    Cap stops  had  to  be added   (refer  to Figure 40  which shows
    hinge  lugs that broke  and were  repaired).

    Since  making  these modifications the  operation of the stand-
pipe  cap  linkage  has  fairly good  reliability,  except for cases
where there  are  interferences with  the  steam valve linkages.

Damper Valve Operating Mechanism

    The damper valve  operating  mechanism did not perform
reliably.  Aside  from alignment troubles, there are two major
problems:

                                119

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        ASCENSION PIPE OPERATING LINKAGE
GOOD CLEARANCE BETWEEN THE LID OPERATING MECHANISM
AND THE STEAM LINKAGE.
                   FIGURE 38
                      120

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         ASCENSION PIPE OPERATING LINKAGE
TIGHT CLEARANCE BETWEEN LID OPERATING MECHANISM AND
THE STEAM LINKAGE.
                    FIGURE 39
                      121

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                   STAND PIPE CAP HINGE LUGS
BROKEN CAP HINGE LUGS THAT HAVE BEEN RE-WELDED. A NUT HAS BEEN
WELDED IN PLACE TO PROVIDE A STOP THAT WILL PREVENT HINGES FROM
BREAKING.
                          FIGURE 40
                             122

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Damper Valve Operating Mechanism  (continued)

1.  The Pullman damper shafts bend, apparently  as  a  result  of
    the impact after the mechanism  falls  free when the  counter-
    weight rotates past the neutral point.

    A damper stop mechanism has been designed  (Figure 41) that
    can be adjusted to take up some of  the  shock that would be
    transmitted through the damper  shaft  as the damper  valve
    strikes the valve stop.  The  adjustment must be  carefully
    made so that the spring receives the  initial impact, but
    that it is not stressed sufficiently  to prevent  a proper
    liquor seal.

    Six of these mechanisms have  been installed and  are being
    evaluated.  It is necessary that the  adjustment  requirements
    do not change with time, otherwise  the  shafts  could be
    damaged before the need for re-adjustment is established.
    There are no apparent problems after  three  months operating
    experience.

2.  There are some stiff dampers  for which  the  damper lever does
    not free-fall as required by  design.  Some  of  these are
    stiff enough that they can not be operated  properly with
    the larry car rotating levers.  When  these  levers become
    this stiff, they cannot be operated from the car, and must
    be moved manually.  About  6% of the  linkages  are in this
    condition now.

    Various means have been used  to free  the dampers.   Several
    types of lubricant including  penetrating oil and flushing
    liquor have been used without success.   A very recent method,
    worked out by J&L maintenance, of spraying  water on the
    damper shaft bearing outside  surface  has succeeded  in free-
    ing fifteen dampers.  The difference  in the expansion
    coefficients of the steel bearing and the cast iron housing
    resulted in sufficient separation to  permit washing with
    penetrating oil.  A final heavy application of lubricating
    grease resulted in a freely operating mechanism.

    When a damper can no longer be operated manually, it must
    be changed.  This is a major  job and  requires  removal of

                             123

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41

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Damper Valve Operating Mechanism  (continued)

 2.   (continued)
     the standpipe.   There have been approximately eleven dampers
     changed since May,  1972.   This will no longer be necessary
     if the water application continues to work.

     Since this problem had not been occurring previously, it
     is believed by  some to be related to the AISI/EPA charging
     system.  One theory is that the basic problem is the result
     of hard tar deposits on the Pullman damper shaft bearings.
     This could be the result of partially plugged liquor sprays
     and/or steam leakage.  The increased steam pressure and gas
     flow rate results in  less cooling  from liquor  sprays during
     charging.   The  tolerance to partially plugged liquor sprays
     is apparently decreased.   The partially plugged nozzle and/
     or steam leakage will result in a localized high temperature
     condition in the collecting main.  This can vaporize the
     light volatiles from the tar deposits which always exist
     in the damper bearings.  When the liquor sprays are cleaned,
     and proper cooling takes place,  the remaining residue of
     tar or pitch in the bearing •_.v-ea becomes very stiff or in
     some cases hard.  This condition can occur as temperatures
     exceed 300° F for prolonged periods of time.  The total
     condition can be further aggravated by the amount of coal
     or coke fines which are combined with the tar.  Once the
     tar deposits start building up on the bearing surfaces the
     condition becomes progressively worse.  Liquor sprays are
     now cleaned on  a weekly inspection cycle.

     There is also the possibility that a bent damper shaft could
     cause the  problem by permitting the damper to be left in a
     slightly open position so that the liquor spray does not
     properly clean  out the t?r deposits from the damper. Since
     some of the- dampers changed did not appear to have bent
     shafts of sufficient magnitude to prevent proper operation,
     at leap's most of the failures cannot be attributed to this
     cause.
                               125

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Linkage Operation

    The ability to control  the operation of the ascension pipe
linkages  from within the  enclosed cab of the larry car is very
desirable.  It minimizes  the  larryman's exposure to the battery
and reduces the lidman's  work.  Achieving reliable operation at
p-4 battery will be a difficult task.  The required millwright
maintenance to keep the linkages in operating condition will
probably  involve 8    man-hours per week.

    In view of the difficulty with interference of the steam
linkage with the lid linkages, the steam linkages will probably
be removed.  The larry car  will then operate the damper and lid
linkage mechanisms.  The  lidman will operate the aspirating steam
valves and the jumper pipe  valve.

GOOSENECK CLEANER

    The original gooseneck  cleaner was never used successfully.
The mechanism required good alignment between the gooseneck and
the charge car to be able to  function.  A survey along the ovens
showed that the distance  between the car and gooseneck (cross-
battery)  varied within a  total band of 4".  The corresponding
elevation varied 3 3/4".  When the car was spotted on the oven
to be charged, the variation  in gooseneck cleaner position and
the gooseneck opening  (oven to be cleaned is two positions south
of the oven to be charged)  is a band of 3".  The cleaner could
not be made to work under this set of conditions.

    The cleaner was relocated on the car to obtain optimum
positioning on a selected group of ovens, but still could not
be used effectively.  The variation of the position at which the
cleaner rested on the bottom  section of the gooseneck opening,and
the resulting difference  in the gooseneck travel angle rendered
the device ineffective.   The  rotating disk and shaft would
strike the inside of the  gooseneck during operation in such a
manner that resulted in it  catching in the spray nozzles.  A
chain ratchet was required  to pull it out.  Since the combined
efforts of J&L and Koppers  personnel were not able to make this
gooseneck cleaner function  properly on this battery, it was
decided to proceed with an  entirely new design.  The remote
operation of a mechanized gooseneck cleaner was an essential
part  of this system.

                               126

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                                                                     GRAM
ro
                                      PARALLELOGRAM

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                   GOOSENECK CLEANER OPERATION DESCRIPTION

    The gooseneck cleaner  assembly is parked in an upstanding position  (not
shown) supported by pivot  axle (4)  and resting pad (5).  In this  position  the
assembly will not fall  forward in case of cylinder failure since  its  center
of gravity  is safely past  the pivot axle.

    Cleaning cycle begins  by  pivoting the assembly by means of cylinder  (1)
from the parked position to down position where the support parallelogram  (5)
reaches resting pad  (20).  The remaining of the cylinder  (1) stroke pushes
the assembly to the forward working position shown here.

    During  forward motion  from the down position to the forward position the
assembly is guided into lateral and vertical alignment with the ascension  pipe
by means of guiding funnel (7)  mounted to the ascension pipe and  indexing  pin
(8) mounted on the assembly.   The length of the forward motion from the down
position to the forward position varies as inside end of funnel stops the
indexing pin to the right  relation with the ascension pipe.

    As the  indexing pin slides against the inside of the funnel and moves  the
cleaner assembly laterally and vertically, the parallel orientation of the
assembly is maintained  by  means of a lateral parallelogram system (9) support-
ing the assembly and a  vertical parallelogram system  (10)  supporting  the lateral
parallelogram system.   Centering springs  (11)  provide additional  help to gravity
for centering lateral parallelogram system.  Supporting springs (12)  support
the assembly through the vertical parallelogram system and can be adjusted
to carry the assembly at a mean elevation by means of adjustment  nut  (13)  at
one end of  each spring.

    Frame  (14) which is carried by the lateral parallelogram system,  supports
the cleaner cylinder (3) through two opposed linkages  (15) and (16).  When
cylinder (2) is moving  the cleaning cylinder (3)  forward by means of  pulling
linkage  (15), linkages  (15 and (16)  are pivoted in opposing curves about their
fixed pivots mounted on frame (14)  causing the cleaning tool (17)   to  dodge
under the upper lip of  the gooseneck opening while advancing from the down
position to the forward position.  (Linkages (15) and  (16) and cylinder  (2)
may not be  necessary when  the gooseneck opening is designed to permit straight
motion of cleaning the  tool from the outside to the inside of the gooseneck.

    The cleaning stroke of the cleaning tool inside the gooseneck as  stated
above is accomplished by stroking action of cylinder  (3).   During the cleaning
stroke of an axially misaligned ascension pipe, the cleaning cylinder is
permitted to be pushed  off axis by means of a spherical joint connection at
linkage  (15) and a spring  suspension system at linkage  (16).  After cleaning,
all above described sequences are reversed to bring the assembly  back to its
parked position.

    Note that when support parallelogram  (6)  is backed up to the  parked position
contacting  surfaces (18) and  (19)  meet to force parallelogram (6)   to  swing
upward about pivot (4) .

                                   FIGURE 43
                                      128

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GOOSENECK CLEANER  (continued)

    Design criteria were determined that would  require  the  goose-
neck cleaner to align itself to the gooseneck with  a  position
uncertainty corresponding to a volume  (5 1/2" vertical,  6 1/2"
cross-battery. 3 1/2" north-south) .  The swab was to  be a cookie-
cutter type, 11 3/4" diameter, and remotely operable.   The  design
is shown in Figure 42 and 43.

    This unit was completely tested in  the fabricator's shop us-
ing the electric, and hydraulic controls and an  actual gooseneck
assembly.  It met all design criteria during the final  shop test
on October 9th.  The unit was received  at J&L in early  November
and will be operationally tested in March.

TRACTION DRIVE

    This drive permits the car to accelerate at maximum rate
within the current limit of 200% load at a smooth bumpless  rate.
It was capable of 400 feet per minute maximum traverse  speed.
It was controlled without difficulty at 2% speed for  accurate
spotting over a charging hole with the  car positioning  system.
The drive system has low backlash so accurate spotting  is possible,

    The performance of this drive system has been excellent and
there have been no serious malfunctions in 16 months  of production
operation and 2 1/2 years exposure on the battery.  Two failures
involving regulator cards have occurred since it was  installed.

    There have been two minor problems with this system:

1.  There were three failures with the  traction drive caused by
    shorted wires to devices located externally on  the  larry car
    that were not actually part of the  traction drive system.
    Those devices such as a warning bell and the stopping sensor
    were removed from the traction drive supplies,  and  now  use
    independent supplies.

2.  At the start of production operation suppression  trip outs
    occurred at times.  These trip-outs are not serious since
    the drive can be manually reset with a push button  in the
    control room.  These were found to have been caused by  poor
    contact between the trolley contact shoe and the 460 volt

                              129

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TRACTION DRIVE (continued)

2.  (continued)
    supply rails.  The tension of the trolley pole was increased.
    Also capacitors were placed at the output of the phasing
    transformer.  There have  been negligible occurrences of
    suppressions in the past  six months.

COAL CHARGING CAR POSITIONING SYSTEM

    The automatic spotting  system was used by the operators
from the start of production  operation in September 1972 through
mid-January 1973.  At the start of operations it was necessary
to adjust the vane positions  on many ovens.  There was no signifi-
cant adjustment of any vane from October  through mid-January.
The stability of the vane position of all ovens is known to have
been satisfactory during that time interval.  The vane limits
(rated 149° F) on the car were occasionally subject to excessive
heat resulting from flames  during charging, which heat up the
heat shield.  One switch failed from excessive heat.

    The positioning system  stopped the car 95% of the time with-
in + 1/4" and almost all times within ± 1/2".  This type of
accuracy is satisfactory.   Figure 44 graphically indicates
typical spotting accuracy data.

    When the car does not spot properly,  the operator can get
around the problem very easily.   He either tries another auto
spot, or he spots manually.   With manual  spotting used (gun-
sight positioning), a pushbutton is operated to tell the control
logic that the car is spotted for charging.

    In mid-January there were two accidents in which vane limits
struck brass vanes.  This caused permanent damage to several vane
limits.  It is .not known how the vanes were bent out of place
sufficiently to strike the  limit.  The vane limit has a "U"
shape opening of 1 1/2".  The brass vane  is 1/8" thick.  It is
possible these vanes could  have first been bent by something
external.  To the extent that this can cause severe damage to
the limits,  the system has  undesirable features.

    There are two significant advantages  in having an automatic
spotting system:

                              130

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                                151

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COAL CHARGING CAR POSITIONING  SYSTEM (continued)

1.  It stops the car in an  optimum position prior to initiating
    a charging sequence which  depends on accurate positioning
    to function reliably.

2.  There are times when  it is difficult for an operator to
    see the proper spotting position, particularly when steam
    from the coke wharf is  present.   With the automatic system,
    this is not a factor.

    In spite of these advantages  in using the system, the problem
of damaging vane limits as  a result of uncontrolled conditions
minimizes the utility of  such  a system.  The operators have the
ability to spot within _+  1/2"  without difficulty in the manual
mode using a gun-sight.   The automatic system is no longer used
at P-4 battery.

    This automatic system can  be  successfully applied if a way
can be found to prevent excessive damage from occurring when
vanes get moved in such a manner  that they strike the limit switch.

HYDRAULIC SYSTEM

    In general the system has  performed reliably.  The pressure
was increased from 1000 psi to 1300 psi to provide additional
force to raise the drop sleeve.   The system can be run contin-
uously without overheating  the hydraulic fluid.  If the fluid
temperature rises above 130° F,  then it is time to look for
excessive internal hydraulic leakage.

    The life of the hydraulic  valves and switches appears to be
satisfactory.  The problems with  the hydraulic system relate to
leaks and hose failures.  The  failures can be minimized by the
judicious combination of  piping with hoses to minimize hose
exposure to heat and flames.   The arrangement must be such that
hoses can be easily replaced if they do fail.

    Few of the original hoses  are still in use on this car.
A "GSM" heat-resistant hose manufactured by Goodall Rubber
Company has performed as well  as  any tested.  This hose has a
double layer of woven asbestos insulation under the armor.
                              132

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ENVIRONMENTAL CONTROL UNIT

    The Environmental Control Unit has been  a  source of high
costly maintenance.  The dual inertia-type dust  louvre  clog
easily and become coated with tarry material which is difficult
to remove, thus resulting in serious  reduced air flow and  sub-
sequent rise in temperature in  the electrical  control room.
Frequency of cleaning varied from two to  four  weeks with
occasional frequency as little  as one week.

    The replaceable bag-type filter had to be  changed every
seven to ten days at a cost of  approximately $50.00 for each bag
plus labor costs.  Because of the design, considerable  time was
spent in removing the access plates in order to  clean or change
the filtering components.

    In an effort to increase the useful life of  the Dust Louvre
and Dri-Pak, a disposable type  filter (FARR  Type 83,  Glass Fiber
Media, Class II) has been installed at the air  inlet of  the system
behind the bird screen.  This filter  must be changed on a daily
basis, but is easily accessible.  Results, today,  indicate that
this pre-filter has significantly extended the life of  the down-
stream Dust Louvre and Dri-Pak.  The  useful  life of the Dri-Pak
appears to have been extended sixteen to  twenty  days.

    The pre-filter has eliminated the tar deposits which clogged
the inertia-type dust louvre.   This unit  requires a monthly
cleaning, but this is much easier in  the  absence of tar.  The
access plates have been hinged  to shorten the  cleaning  or
replacement time.  Additional work is planned  to improve the
filter to further reduce required maintenance  and improve the
over-all removal of particulates.

Charcoal Fijlter:

    Despite efforts to evaluate the useful life  of the  activated
charcoal filter by means of acceptable analytical techniques
(% activity, % retentivity, % volatile content,  etc.),  no success
has been achieved in deriving an evaluation  procedure.   The
carbon steel housings of the charcoal trays  corroded to such an
extent that it was necessary to replace them with stainless
steel trays.  Subsequently, these replacement  filters became
clogged with deposits of ammonium sulphate which not only

                               133

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charcoal Filter (continued)

eliminated the effectiveness of  the  activated carbon but
significantly reduced the  total  air  flow through the system.

Specification Deficiencies

    Performance evaluations made on  this system indicate that
it failed to meet the following  specifications:

1.  THE TIME-WEIGHTED AVERAGE  CONCENTRATION OF 0.2 MG/M3 OF COAL
    TAR PITCH VOLATILES  (BENZENE SOLUBLE FRACTION) SHALL NOT BE
    EXCEEDED DURING THE NORMAL 8-HOUR WORK DAY.
    Environmental measurements made  inside the larry car indicated
    the average time-weighted  concentration of Coal Tar Pitch
    Volatiles (Benzene Soluble Fraction)  in an 8-hour work day to
    be an average of 0.73 mg/M3,  ranging from 0.3  mg/M3 to 1.02
    mg/M3.

2.  99.9% REMOVAL OF PARTICLES BY FINAL FILTER, DOWN TO ONE
    MICRON PARTICLE SIZE.
    Environmental measurements made  inside the cab indicated
    the overall system efficiency to be 86.3%.

3.  THE TIME-WEIGHTED AVERAGE  CONCENTRATIONS OF CO SHALL NOT BE
    EXCEEDED DURING THE NORMAL 8-HOUR WORK DAY.
    No provision has been made for removal of CO in the
    Environmental Unit.  Environmental measurements indicated
    that the time-weighted average concentration of 50 PPM was
    exceeded at least one of three working shifts  sampled.

4.  THE VENTILATION UNIT SHALL PRESSURIZE THE OPERATOR'S CAB 0F
    THE COAL CHARGING CAR.
    Measurements made inside the operator's cab indicated no
    significant positive air pressure.

    With the lack of a weighted  final louvre, perforated ceiling
    tile in operator's cab, and  an unbalanced ventilation system,
    pressurization of the cab  would  require increasing the air
    delivery over its present  capacity .
                              134

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Conclusions

    Although  the  system did  not meet all the specifications,
the working environment in this enclosed larry car cab is a
significant improvement over an open cab.   The location of the
unit on  the larry car  at the pusher side of the car exposes the
air inlet  to  pushing emissions.   It had to be located there
because  of space  considerations.  If space were available on the
opposite corner of the car (Eig.9-Pg.33)  where the hydraulic unit
is shown,  its reduced  exposure  to emissions would significantly
improve  the performance.

ELECTRICAL SYSTEM

    The  collector rail system has been very adequate for the new
larry car.  The stainless steel has proved to be superior to the
plain carbon  steel rails.  When the car travels along the battery,
the static on the radio communication system is very pronounced
at the plain  carbon rail section and quiet at the stainless
section.   High speed recordings of the supply voltage on the
car indicate  a much steadier voltage from the stainless steel
portion  of the rails,  as a result of superior contact with the
collector  shoes on the car.

Larry Car Logic

    The  sequencing control consists of solid state logic with
outputs  that  control standard industrial solenoid relays.  The
logic control is  divided into two sections - Automatic and
Manual.  These sections were made as independent as possible so
that a fault  in one would  not be likely to affect the other one.
They share input  sensors (limit switches)  and output relays.
An AUTO-MAN switch at  the  console permits  the operator to
select the sequencing  mode.   There have been many AUTOMATIC
charges  made  in which  it was necessary to  switch over to MANUAL
mode to  complete  the charge.

    After  considerable operation on the system,  it is believed
that two independent logic sections are not necessary.  Each
logic cabinet has  its  own separate power supply.   The equipment
has proved to be  reliable  and separate power supplies are not
necessary.  If a  relatively  complex manual system of logic is
to be furnished,  similar  to  what was required on this larry car,

                              135

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 Larrv Car Logic  (continued)

 along with an automatic  system that simultaneously or sequentially
 initiates the various  sub-operations,  then the logic should be
 sectionalized as a minimum separation.  The MANUAL logic  should
 all be in separate independent sections.  The AUTOMATIC logic
 would then provide initiating signals to the individual MANUAL
 logic functions.  The  MANUAL functions would supply signals
 to the AUTOMATIC  indicating the status of completion.  This
 arrangement would be simpler, and require less hardware than
 used on the AISI larry car.

    Test switches were provided so that the logic sequences
 could be stepped through for trouble shooting purposes.   These
 proved to be difficult to use effectively.  Trouble shooting
 has been accomplished  by observing the status indicating  lights
 as the equipment is operated, usually at the south end of the
 battery in a "test" position.  Other necessary tools are  a volte-
 ohmeter to measure logic voltage levels.  When a multiple choice
 of events can cause the  trouble, logic elements can be grounded
 to COMMON to narrow down the possible sources of trouble.

    The performance of the logic has been reliable.  This is
 attributed in a  large  measure to the way in which it was
 designed and manufactured by General Electric.  Logic level
 power sources and the  COMMON lines are sufficiently heavy to
 maintain adequate levels.   There have been few problems with
 inadequate contacts.   One question raised in the initial  design
 stages, related to the  application of logic, was its performance
 in a coke oven atmosphere.   To date there has been no general
 problem that has been  caused by the oven environment.  Connectors
 of the plug-in cards have a  tin-nickel alloy plating.  The
 connection at the card plug-in point is designed to be gas-tight.
 General Electric states  that this type of connection has  been
 tested in their  laboratory to ensure its ability to withstand
 corrosion.  This test  consisted of three weeks in a 5% I^S
 atmosphere over water.

    The low voltage relays that furnish outputs from the  logic
 are hermetically sealed.   The fact that the logic equipment is
 designed to operate in an industrial atmosphere does not
 preclude the necessity to protect the hardware.  The air  must
be conditioned.  It is desirable that the temperature be

                              136

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Larry Car Logic  (continued)

controlled well within  design  limits  so that local hot spots or
marginal operations  are avoided.   The equipment must be enclosed
and requires careful periodic  cleaning with a vacuum.

    In an effort  to  ensure  continued  equipment reliability the
logic control  is  insulated  from the outside world by using an
isolation input element which  has  no  electrical wired connection
between input  and output.   The input  sensors are applied at a
voltage level  of  105 V.D.C.  There were a  few problems associated
with this device.  It is mounted on a stationary back plate
from a terminal block.   There  were occasions when a soldered
terminal developed a crack  which resulted  in intermittent mis-
operation.  The terminal board has since been re-designed by
the supplier to provide a stronger mechanical joint and increased
solder area.   There  were also  several failures of the device
itself caused  by  a poor solder connection  to a transformer.
This was a weakness  in  the  design  and has  since been corrected
by a modification.   There have been no other types of troublesome
logic elements, and  the overall performance has been good.  The
output relay cabinet and the magnet controller cabinet contain
standard industrial  equipment  that has performed well.

Electrical Equipment Reliability

    In general the reliability of  the equipment in the control
room has been  good,  and  the required  maintenance is minimal.
The major problems have been related  to the equipment outside
the control room.  The  sensors have been the least reliable
part of the electrical system.

    The following is a  list of required external limit switches
for control purposes on this car.
                                                       TOTAL
1.  Lid lifter                        (5)                 15
2.  Butterfly  oscillate              (3)                  9
3.  Feed hopper position             (3)                  9
4.  Coal level sensors                (1)                  3
5.  Ascension  pipe linkage  operators  (4)                  4
6.  Gooseneck  cleaner                 (2)                  2
7.  Coal bin gate operator            (2)                 __2_
                                                         44
                               137

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 Electrical  Equipment  Reliability (continued)

    The lever operated  switches could not survive any exposure
 to flame.   There were also  problems with the operating levers
 sticking, or becoming loose.   The lever operated limits  (coal
 bin gate excepted) were changed to a "GO" - type proximity switch
 rated at 450° F supplied by General Equipment and Mfg. Company.

    The application of  this switch to sense feed hopper position
 did not improve the reliability to the extent desired.  An
 improved heat shield was fabricated, and the reliability has
 been good since that time.   There have been no problems since
 the proximity limits were installed on the ascension pipe
 linkage lever arms actuators.

    The applications of this  limit to the lid lifter did not
 improve the reliability to  an acceptable level.  The switches
 were still  exposed to flames  which caused failures.  A recent
 improvement has been to wrap  them with a high temperature
 insulating  material as  shown  in Figure 45.  The purpose of the
 insulation  is to prevent heating the switch above 450° F,  This
 modification to switches on #3 hopper and #3 lid lifter has
 not had a sufficient test period to evaluate.  At this time
 there have  not yet been any failures  (3 months operation).

    The limit switches  were applied in two different types of
 circuits.   All sensors  that indicate equipment is in the "Travel
 Position" permitting the larry car to move, are part of the trac-
 tion drive  control.  The supply voltage used in these control
 circuits is 115 volts a-c.  These limits actuate relays with
 contacts  supplying not only  the necessary traction drive relay
 control, but also the sequencing static logic at 105 volts d-c.
 This creates two problems:

 1.  When electrical repairmen are working on limit switches
    they must de-energize both power supplies to remove to a
    potential hazard.

 2.  If multiple grounds occur in the sensors, there can be
    cross currents occurring  between the 115 V.A.C. circuits
    and the 105 V.D.C.  circuits that give unpredictable results.

A preferred method of design  would have all sensors  on the same
 supply circuit.
                               138

-------
U)
                           O?
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    3IMITCH'.
2.  JAl&APA a OUT Two To
          &JHTSTCH.
                                                  To
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                                                          THJS

-------
electrical Equipment Reliability  (continued)

    The  service  life  of the Bin-0-Matic type sensor  (75% coal
 level) ,  which  is  used to indicate when leveling  is to be
 initiated, has been adequate.   Details of this device are
 discussed  on page 107,  Hopper Level Control.

    The  vibrators have a past history of failures.  Most of  the
 failures are believed to have been caused by wear in the bear-
 ing housing.   Some  of the failures are known to  have been caused
 by excessive exposure to flame.  The relocation  of the vibrator
 on the hopper  appears to have eliminated the excessive failure
 rate.  Also the  later style Martin Motomagnetic  rotary electric
 vibrator model DVE-3500 is being replaced by an  earlier  style
 of the same mode.   The earlier style apparently  has better
 mechanical features.

    The  traction  drive mill-type d-c motors, complete with
 permanent  magnet  type tachometers have required  no repairs to
 date.

    The  performance and reliability of the external equipment
 will be  considered  acceptable if the life of the insulated
 proximity  switch  meets expectations and the vibrators continue
 to hold  up well.

Larry Car - Pusher Machine  Alignment

    Originally a  gamma ray interlock was considered.  This system
 consisted  of two  sources of Cesium 137 enclosed  in a shuttered
 holder so  mounted on  the existing pusher as to direct two
 collimated gamma  ray  beams to receivers on the larry car.
 Because  of beam  interference from the raw gas cross-overs, two
 pairs  were required to ensure a clear sight line.  Jones &
 Laughlin declined to  use the system because of the necessary
 operating  and maintenance requirements to comply with A.E.G.
 regulations.

    The  interlock actually furnished was an Ultra High Frequency
 system operating  at a frequency of 10.2 GH2/ with a specially
 designed compressed antenna system.  The arrangement is  shown
 on Figure  21,  page 53.


                              140

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Larry Car - Pusher Machine Alignment  (continued)

    The system was developed to operate with the  following
design considerations:

1.  Extreme variations in heat and atmospheric conditions.

2.  Must operate through the existing and available line of
    sight conditions between the larry car and pusher machine.
    The line-of-sight conditions stipulated that  an 8" x 8"
    opening was available at every oven, but that due to lack
    of perfect alignment between the machines, the system must
    operate with a 6" x 6" clear opening.

    The following design factors are related to signal
conditions:

1.  The transmitter must develop enough power to  low voltage
    levels to maintain a signal variation of 10 to 1.

2.  The received signal must be adjustable to recognize a 500
    micro-volt level for the pre-set distance of  20 feet.

    The transmitter (48" long x 5" wide x 5" high) is mounted
on the pusher machine with the antenna alignment  designed
for an 8" square opening between the pusher and larry car.
The transmitter oscillator is an integral part of the antenna
system.  An indicating meter provided the operator with visual
information that the transmitter was working.

    The receiver (48" x 5" x 5") is mounted on the larry car.
The antenna is a specially designed compressed type with a gain
of about 4db.  The antenna is coupled to the receiver by a wave
guidesystem.  The wave guide is a non-pressurized type.  The
receiver operates into a dc amplifier which provides an output
voltage proportional to the received signal level.  The amplifier
drives a relay.

    This system was checked out initially in a test position at
the south end of the battery.  It functioned properly at that
time.  No attempt was made to place it in service until the charg-
ing system was in operation.  During this interval of time the
equipment was severely damaged by the heat from burning gases.
                              141

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Larry Car - Pusher Machine Alignment  (continued)

The transmitter on the pusher,  and the  receiver and wave guide
on the larry car would have  to  be replaced or completely re-
worked.  The large expense involved in  repairing the system
could not be justified, especially since it was not suited to
the environment.

    It was also determined that the maintenance of an 8" x 8"
opening at every oven would  be  very difficult.  A preliminary
survey, made before the larry car was built, had indicated that
such an opening could be realized by moving certain obstructions,
A later survey made with the actual equipment indicated that
this could be done on approximately 90% of the ovens.  The
exact position of the pusher and the larry car with respect
to the opening is subject to some variations with time.  This
system is not recommended for use as an alignment interlock.

    Using single spot pushing and charging on the pusher machine
and having available a voice communication system between the
two operators minimizes the  chance of charging the wrong oven.
It does not prevent a larryman  from starting a charge prior
to the presence of the pusher machine.   The problems involved
in relying on proper operating  procedures versus the maintenance
expense and additional time  required to use the available inter-
lock systems must be .carefully  weighed  in making the decision
whether or not to use one.

Operating Modes

    The AUTOMATIC and MANUAL operating  sequences are described
in Section V beginning on page  24.
Automatic System -

   The AUTOMATIC sequence has  not  been used extensively.  The
principal problem is associated with the reliability in operation
of the charging system components.   The single AUTO CHARGE
operation was not used because  of reliability problems with the
ascension pipe linkages.  Movement  of lever #2 to the UP position,
as determined by a limit switch, did not guarantee that the
linkage systems had been properly operated.  With prepare-to-feed

                            142

-------
Automatic System-(continued)

conditions  satisfied,  such  as  lever  #2  UP,  the charging of coal
was initiated.  However  if  the oven  was not on-the-main (damper
not open or standpipe  cap not  closed, or aspirating steam not
on),  it required  some  fast  moves  on  the part of the operator to
correct the malfunction.

    The automatic  system was difficult  to use continually with-
out reverting back to  the manual  mode of operation.   The largest
single factor was  the  lack  of  reliability in the coal feed
system.  The automatic mode initiates operations simultaneously
or sequentially depending on the  successful completion of
previous events.   The  start of an automatic sequence,  such as
AUTO  FEED,  requires that related  charging equipment be properly
positioned  initially.  Once an operation starts,  it can be
canceled only by going back to MANUAL operation.   If the coal
flow  fails  to start in #2 hopper,  the butterflies of #1 and
#3 are closed until the  flow in #2 is started.   This requires
switching to the MANUAL mode in order to close #1 and #3
butterfly.

    If a butterfly stalls because the coal  backs-up the charging
hole  during leveling.  The  AUTOMATIC mode would continue to
attempt to operate the butterfly.  This increases the chances
of packing coal in the drop sleeve.  With the manual mode the
butterfly operation is terminated until the leveler bar removes
enough coal.

    Failure of a butterfly  valve  to  close sufficiently to sense
it with the limit  prevented raising  the drop sleeve to
complete the automatic operation.  Another  problem was not
getting all three  drop sleeves UP when  they were raised.   This
happened if there  was  too much coal  left in the hopper.   With
MANUAL  control the drop sleeves  would  be lowered again,
the butterfly valve oscillated to charge the excess coal,  and
then  raised.  When charging with  wet coal having 8% or more
moisture, it is a  normal procedure to empty excess coal from
the drop sleeve to minimize the chance  of coal packing on the
next  charge.  There were so many  instances  where MANUAL operation
was required, that it  was impractical to charge with the AUTO
mode.
                               143

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Automatic  System-(continued)

    Another problem  that  was manifest with the use of the
AUTOMATIC  system was its  inflexibility.  The sequence of
operations was  frequently changed in order to determine the
best charging procedure.   The time at which the leveler bar
entered  the oven was changed.  The leveler door was closed prior
to re-lidding.  Different charging procedures could be tried
MANUALLY with no difficulty.   Changed procedures with the
AUTOMATIC MODE  would require changes in the logic.

Manual System—

    All  charging operations are now done with the MANUAL mode.
Indicating lights are provided so that the operator can monitor
the performance of the operation.  Each lid lifter has lights
indicating the  EXTEND,  RETRACT, UP,  DOWN position, LID OSCILLATE
motion,  LID IN  CONTACT WITH MAGNET,  and MAGNET ON-OFF.  Without
actually seeing the  motions,  the operator can definitely determine
that a lid was  actually removed and/or replaced, that the operat-
ion was  properly sequenced,  and that the lid lifter is in the
travel position (UP  and RETRACTED) .

    Sequencing  of the lid lifter operation is subject to
occasional failures  in some part of the system, particularly
sensors.  An Emergency-Manual sequence is provided whereby
individual motions can be initiated independent of the limits.
The operators use this feature successfully.

    Additional  lights indicate the drop sleeve position (UP-DOWN),
butterfly valve (CLOSE, OSCILLATE CW, OSCILLATE CCW),  damper
levers (UP-DOWN), coal level (TOP, 75%, EMPTY), vibrator (ON),
and coal bin gate  (OPEN,  CLOSED).  With these lights the operator
can determine the status  of the various mechanisms, even when
they can't be seen.

    With training the operators have been able to use the MANUAL
controls without difficulty.   The application and performance.
of the MANUAL controls is considered to be successful.

Successful Automatic  System -

    The approach to  a  successful automatic system first requires

                             144

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Successful Automatic System-(continued)

a successful manual system.  After  the  development of a
consistent reliable manual  system,  then it  would be feasible
to attempt an automatic  system, provided the  gains of automation
warrent the expense in achieving  it.  It is believed that  the
basic approach used on this  system  could be successfully applied
under those circumstances.

Carrier Current Signal System

    The AUTOMATIC operation  required  the use  of the control
signals between the charging machine  and the  pusher machine
utilizing a carrier current  pulse code  modulated system.

    This transmission system requires the use of a way-side loop
for the charging car, and a  second  loop for the pusher machine.
Originally as installed  these two loops were  one continuous
loop.  The signal losses at  the pick  up coil  of the receiving
machine proved to be too large for  reliable operation.   A
repeater station was installed at the north end of the battery
to minimize the losses.  The signal at  the  repeater station is
amplified so that it is  re-transmitted  at the same level as
originally sent.  It is  necessary that  the  frequencies be
different so that only one transmitter  and  receiver work together.

    This is the first application of  such a system to more than
one moving vehicle.  The system worked  reliably as long as the
equipment outside the control rooms was working properly.  The
principal problems were  related to  equipment  damage as a
function of its exposure to  fires.  The coaxial cable which
connects the larry car antenna to the radio equipment failed twice
This type of cable is very sensitive  to heat  and it was
necessary to reroute the cable so that  its  conduit was not exposed
under the car.  The coaxial  cable which connects the pusher pick-
up coil to the radio receiver also  experience heat problems in
the vicinity of the pick-up  coil.

    The wayside loop on  the pusher  side was located under the
collector rails.  The way-side cable  supports were exposed to
flame from an open chuck door.  These supports would bend and
cause the cable to be out of proper alignment and interfere with

                              145

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carrier Current Signal System (continued)

the pusher travel.   If the  automatic system is to be used
consistently, this way-side loop must be re-located.

    There were some  initial problems with card failures within
the pusher machine resulting from intermittent grounds.  The
power supply for the pusher machine is 250 VDC.  Digital COMMON
is related to this supply.   This indicates one positive advantage
in using the system  with  a  115 volt a-c supply where transformer
isolation and grounding of  COMMON can be done without difficulty.

    Some additional  logic cards failed in the pusher controls
because the temperature inside the controller exceeded the
rating.  This was corrected by addition of a vent in the ceiling.
A temperature thermostat  was connected to an annunciator.

    It is believed that this system can be made to function
reliably if the external  equipment (antennas,  pick-up coils,
wayside loop, coaxial cable)  can be adequately protected from
excessive heat and system grounds.

Voice Communication  System

    The performance  of the  systems has been good, particularly
the larry to pusher  system.   The battery communication system
at times is hard to  hear  because of a higher noise level.  Its
performance is considered acceptable, and the higher noise level
is partly caused by  the original existing system.  The hardware
utilizes transistorized circuits.
PUSHER MACHINE

Leveler Bar

   After 15 days of operation,  the new bar failed by becoming
distorted so that the  front  end  raised approximately 6 1/4",
starting 20' back from the nose  (Figure 46) .   At a distance of
about 10'  from the nose  two  top  bulb sections of the bar buckled.

   Based ort a conclusion that the top of the bar overheated from
oven radiation, while  the bottom,  riding on coal remained

                              146

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                OPEN WEB LEVELER BAR
OPEN WEB BAR SHOWING THE BUCKLING ON THE UPPER SURFACE
ABOUT 10' FROM THE NOSE.
                     FIGURE 46
                        147

-------
T.eveler Bar (continued)

relatively cool a new design was  made eliminating the side cut-
outs to improve the heat transfer from top to bottom.  A section
of this later design, still using bulb angles for high strength,
are shown on Figure 47.  The bar  was installed on May 20th and
failed on July 16th by rising  about 8 1/8" in the first 23'
back from the nose.  Refer to  Figure 48.

   J&L Research investigated  the problem and concluded that
the bar failure in bowing up at the end was caused by excessive
temperature differential between  the top and bottom of the bar.

   The original bar has twice the web thickness as the self
supporing bar design, and consequently better heat transfer
characteristics.  A study was  made of this bar to determine if
it could be safely used in the AISI/EPA system.   An analysis of
the allowable stresses in the  original bar design indicate
that the bar is self-supporting in use up to a maximum operating
bar temperature of 1100°F.  It was found from test data that
the leveler bar temperature will  not exceed 1000°F if the
initial temperature does not exceed 800°F and the leveling time
does not exceed 3 minutes.  Refer to Appendix C for details
of the leveler bar investigation.  The original leveler bar
has been in continual use since July 16,  1971.  On May 2,  1973
it bent up about 6" in a manner similar to the previously
described failures.  At the time  of failure a different larry
car was in service and the leveling time was assumed to have
been excessive.  Koppers was requested to investigate a leveler
bar design that would be less  sensitive to prolonged exposure
times in an oven.  The results of their study recommended the
use of a bar material corresponding to ASTM A-517-68, grade K
quality, which manifests high  yield strength at elevated
temperatures.  Cost data is shown on table 14, page 185.
                             148

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Leveler Bar  (continued)

    The cost data in Table 14  is given  for  grade  J steel  which
differs from grade K essentially in having  a  lesser amount  of
manganese  (.41-.74 versus 1.05-1.55).   Either of  these  grade
steels has a yield strength of approximately  20,000 psi or  better
at 1150°F.  Grade-J steel may be readily welded in thicknesses of
1 inch without pre-heat, provided the weld  heat input  is  at least
30,000 joules/inch.  Grade-K steel does not require pre-heat in
1 inch thickness for typical compositions,  but if the carbon and
manganese contents are close to the maximum,  a weld heat  input
of 60,000 joules/inch, or 200°F pre-heat may  be required  to
assure freedom from heat affected zone  cracking.

    Improved heat transfer characteristics  (top to bottom)  might
be realized using wedge shaped side plates.   Instead of having
a rectangular section of 3/4" x 10", without  changing the weight
or area, the top thickness would be increased by  5/16 and the
bottom thickness would be decreased by  5/16 (Figure 49).  This
concept has never been tested in actual service.   The use of a
leveler bar of the conventional design but  utilizing the  improved
material would be this writer's preference.

    The proper use of the leveler bar is required to minimize
emissions.  The stroke of the leveler bar was automated so  that
                               149

-------
 T3UL/15
CROSS SErCTio:M
          4-7
      ISO

-------
            SOLID WEB LEVELER BAR
SOLID WEB LEVELER BAR SHOWING THE VERTICAL RINSE
AT THE NOSE END

                  FIGURE 48
                     151

-------
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    49
152

-------
Leveler Bar  (continued)

it would always  extend  to  the  maximum stroke into the oven and
then cycle with  a  9  foot stroke  and  provide maximum leveling under
#3 charging  hole.  The  leveler bar makes about 8 cycles in a
minute or about  135  ft./min. average.   With the addition of jumper
pipes, the leveling  will be done under #2 charging hole, and
the automated  stroke will  be increased to about 20 feet.

    Efforts  were made to increase the  gas passage way in the
oven during  leveling by cutting  about  2" from the top of baffles
between the  3/4" side plates,  and 3"  from the top where the
plates are 1"  (refer to Section  VI,  page 72).

LeveJLer Bar  Smoke  Shield

    The smoke  shield was replaced in July,  1973,  by one with a
modified design.   The leveler  bar used to bind inside the smoke
shield partly  because the  leveler bar  can bend slightly during
normal service,  and  partly because the smoke shield side plates
buckled from the heat.  The top  of the original smoke shield had
to be opened up  to provide adequate  clearance.   The present
smoke shield has inside dimensions corresponding to 9" in com-
parison to the original 8  1/2" opening (leveler bar is 8" wide).

    The leveler  bar  had a  tendency to  even catch the side of
the later model  during  leveling.  This would pull it back away
from the oven.   The  counterweight which forces it against the
leveler door would cause it to return  at great force when
released and would hit  the door  frame  with excessive impact.
A device was made  and installed  by J&L maintenance that will
prevent the  smoke  shield from  being  pulled back more then 1"
during normal  leveling.  A method has  to be found to prevent
this 1" opening  during  leveling.  There are some emissions
from this port during charging (single  gas  off-take).

Leveler Door Operation

    Originally the intent  was  to open  the leveler door manually
while the pusher side door was on the  extractor.   Stop detents
were provided  to hold the  door in the  open position so that
when the pusher  side door  was  replaced on the oven, the leveler

                               153

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Leveler Door Operation  (continued)

door would remain open  so that an air draft would decarbonize
the standpipe.  Later when the oven was to be charged/ the pusher
machine  smoke  seal would  be placed against the open leveler
door. After charging the operator would then close the leveler
door.

    In actual  operation the detent pins would not hold the door
in the proper  position.   Many of the detent holes were not
drilled  in the correct  location.  A revised operating procedure
was worked out to by-pass the problem.  The door is manually
opened on the  extractor and then relocated without latching, with
the back of the cam  on  the handle touching the hook plate mounted
on the door.   This leaves sufficient opening for standpipe de-
carbonization, and requires only that sufficient door friction
hold it  in place.  When the oven is ready to charge, the "door
open" sequence is used.   The mechanism is able to open the door
from this position,  if  the cam stays in contact with the hook
plate.   This was accomplished by adjusting the operator timing
to over-lap the closing and latching motions so that the
operator pin is not  raised behind the door loop.

    There were many  problems encountered in the initial operation
of this  device.  During November, 1971, a Koppers representative
reviewed all problems involving the failure to operate properly,
and corrected  as many as  possible.   Previously, a 3-inch latch
cylinder had been replaced by a 4-inch latch cylinder to provide
additional latching  force.  The major causes of mis-operation,
as determined  by Koppers,  were as follows:

1.  Improper fabrication  of some of the leveler doors which made
    latching of doors difficult, and caused interferences in
    some cases.

2.  Measured distances  between the door opener unit and the
    doors varied up  to  a  maximum of 4" both laterally and "in
    and  out".  The unit was designed to operate within a 2-
    inch square.  The variation in relative spacing can be the
    accumulated errors  caused by:

    a)   Differences  in  rail elevation, or bowing of pusher
       machine rails.

                               154

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Leveler Door  Operaticm  (continued)

    b)  Expansion of the battery.
    c)  Variations in placing of doors  on  the  oven.
    d)  Variations in spotting the pusher  machine (one spotting
        position is used for the door extractor,  pusher ram,
        leveler bar).
    e)  Door  operator may not be located in  the most  optimum
        position.

3.  Tar deposits on the inside of some  doors caused difficulty
    in closing  (ovens were on long coking  times when  this check
    was made).

    As a result of this investigation,  the chuck  door operator
was relocated to an optimum position.   The hook and hook pocket
were ground on about 50% of the doors to facilitate closing and
latching.

    The adjustments on this unit must be very  carefully made to
insure proper operation on all doors.   This  is related to the
variation in  the position of the operator  with respect to the
door.

    More recent problems involved the replacement of  leaking
air hoses.  The original hoses were rated  for  a maximum of 200°F.
Those hoses cannot survive that environment.   J&L replaced them
with the "GSM" heat-resistant hose.  Hose  performance is now
considered satisfactory.
    The engage pin rotate return spring has a  tendency to lose
its spring force as a result of the exposure to  flame.  This
spring has been replaced twice.

    The chuck doors are now lubricated every six months to
minimize the force required to operate them.

    While pushing an oven, an air  jet at  the top of  the pusher
ram is directed at the oven roof to remove as  much carbon as
possible.  The amount of air used  during  this  operation causes
a 20-30 psi drop in air pressure.  The leveler door  operator
uses the same air source.  The door closing operation takes

                               155

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 Leveler  Door Operation  (continued)

 place just after pushing, before the air compressor has sufficient
 time to  restore normal  pressure.  The drop in pressure reduced
 the available door closing  force sufficiently to prevent
 consistent proper closing of tight doors.  An auxiliary air
 storage  tank with a check valve was furnished just for the leveler
 door operator that maintains sufficient minimum pressure at
 all times.

    There have been some problems with the seal of the leveler
 door. The spring which forces the edge of door to seal around
 the leveler door frame  is not designed for the high temperatures
 encountered on this battery.  It has an upper temperature range
 of approximately 425° F.  The springs are subject to 500° to
 800° F  with the heat shield on the door.

    A program is underway to check all leveler door springs when
 the pusher side door is removed for maintenance.  If the leveler
 door spring has a permanent set of 1/8" or more, the spring is
 replaced.  In all cases, a  1/8" asbestos gasket is installed
 between  the door and the spring.

    The  performance of  the  leveler door operator is now
 considered satisfactory.
BATTERY MODIFICATIONS

.Steam Ejector System

    The development of  an  ascension pipe design that functions
as an efficient steam ejector  was the primary goal of an extensive
test program.  The design  effort was limited to apparatus which
could be installed without requiring oven or gas collecting main
modifications. Eight models representing four major ascension
pipe designs were tested on operating ovens at P-4 battery.
These tests  (Figure 50 ) consisted of measuring the air flow
through one open charging  hole in an empty oven (693 cu.ft.)
as a function of steam  pressure and temperature at the high
pressure side of the steam nozzle.  The charging hole lids and
the standpipe cap were  sealed  with mud.  High pressure super-heated


                               156

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                                   OvErlsL  TE.S'T.S
                                                           •TE1VIPE R-AT U R E.
     ORIFICE- FLOW
CJ1
                                    AMD
                                            5O

-------
steam Ejector System  (continued)

steam  (200 psig, 500° F) was  supplied from an auxiliary 4"
header.  A test run consisted of  taking vacuum measurements and
air flow measurements with  different size nozzles at various
steam pressure settings.

    Tests made on the existing ascension pipe were used as the
basis for comparing new designs.   The air flow test results for
the four major designs are  shown  in Figure 51.  The air flow
measured by the orifice flow  meter is shown as a function of
thrust.  The relation between thrust and pressure is given in
Appendix E, along with the  air flow equation.

    The most efficient ascension  pipe (design D) was a ceramic
lined venturi-shaped standpipe with a steam nozzle made from
2 inch, double extra heavy, #316  stainless steel pipe. During
every test the oven vacuum  would  reach 706" of water gage with
approximately 95 psig steam,  and  would not go higher.  Since the
pressure transducers were capable of reading 8" of water gage
vacuum, it indicated a limiting condition of oven vacuum.  At
steam pressures above 125 psig the standpipe cap had to be
held down.

    It was left, in normal service (used original existing steam
nozzle) to determine the life--of  the venturi steam ejector
materials.  After a couple  of months the venturi steam nozzle
was burned and no longer operable.  More development work would
be required to make a production  model.

   , Design "B" used a modified version of the existing goose-
neck with a lined standpipe extension.  The location of the
steam ejector was improved  over the existing design.  The liquor
sprays were relocated so they washed the walls of the return bend

    Design "C" included the improved features of liquor spray
relocation, smooth flow geometry  and a concentrically located
steam nozzle.  The carbon formation in this design was less than
in the existing design "A", or the modified design "B".   The
steam ejection performance  is slightly improved over design "B".

    Tests were performed to determine the equivalent gas flow


                              158

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                 ASCENSION PIPE EJECTOR PERFORMANCE
            2400

            2200

            2000

            taoo
          Jj 1600

          J MOO
          u
          i 1200
          3
          •»• 1000
          •
          5  800

             600
           »
             400

             200
                STEAM TEMPERATURE
                500° F AT 200 PSlG
tt BO
                                   4*  64 62 TO  THRUST LB,
                O  K)  40 10  10  tOO 120 140 160  ISO PRESSURE P»»
                                 STEAM
          •TEAM
DESIGN "A" REPRESENTS THE EXISTING DESIGN
DESIGN "C" REPRESENTS THE NEW DESIGN
ALL DATA TAKEN USING 5/8" STEAM NOZZLE.  PRESSURE MEASURED AT STEAM
NOZZLE. AIRFLOW MEASURED WITH ORIFICE FLOW METER AT #2 CHARGING HOLE.
                              FIGURE 51
                                 159

-------
steam Ejector Sy;sj:em  (continued)

required  to contain emissions during normal charging.  High
pressure  steam was  connected to the ascension pipe, and
emissions during  charging were observed.  Since the oven openings
were not  sealed,  an equivalent test could not be made.  Based on
these observations  a  minimum gas flow of 1500 SCFM appeared to
be required to charge a properly sealed 700 cubic foot oven at
a 90 second charging  rate.

    The air flow  data shown on Figure 51 is based on a 5/8" steam
nozzle.  In order to  use the existing ascension pipes without
modification  the  steam nozzle size was increased to 3/4".  For
a given pressure  this would increase gas flow as much as 40%.

    Super-heated  steam was provided from a 4-inch header at 175
psig and  450° F.  A pressure reducing station was supplied so
that the  steam pressure could be adjusted to the optimum valve.
The piping to individual goosenecks was sized to provide 160
psig at the high  pressure side of the steam nozzle.  From the
data of Figure 51,  this corresponds to approximately 1200 SCFM
for a 5/8" nozzle or  up to 1680 SCFM with a 3/4" nozzle.

    Five  ovens were equipped with design "C"   ascension pipes
so that a performance comparison could be made with, the exist-
ing goosenecks.   The  steam nozzles were made 11/16" diameter to
obtain  similar gas  flow as the original design "A" goosenecks.

    The new design  gooseneck did result in minimal carbon
formation.  The carbon deposits were normally soft and easily
removed.   The operating personnel did not like cleaning these
goosenecks because  they were higher and not accessible  for manual
cleaning  in a conventional manner.

    The flushing  liquor spray connections were not as easily
cleaned as the original ones.  This part of the design should be
revised for easy  removal by non-skilled employees, rather than
requiring a craft such as a pipefitter or millwright.

    The steam aspirating qualities of the new goosenecks are
similar to that of  the original design (the existing goosenecks
use more  steam since,  the nozzles are larger) and consequently

                              160

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 Steam  Ejector  System (continued)

 the  new  design will  be  removed so that only one type is used.
 The  mechanized gooseneck cleaner  can be used only on the exist-
 ing  type ascension pipe.

 Clean  Ascension Pipe -

     The  passage way  for the  gases must be maintained open.
 Carbon deposits must be removed from the standpipe and gooseneck.
 When less than 80% of the opening is clear,  the effect on oven
 aspiration usually is noticeable.

     If the normal decarbonization cycle does not result in
 removing all the carbon deposits,  the standpipe must be kept
 open by  poking the carbon loose with long steel rods inserted
 from the top inspection cap.   The gooseneck  is  cleaned prior
 to charging with a swab.   An operating mechanized gooseneck
 cleaner  will help this  operation.

 Self Cleaning  Steam  Nozzles -

     The  self cleaning steam nozzles  installed on P-4 battery
 had  three  significant problems:

 1.   The  rod broke on  several of the  nozzles  where the cotter-
     pin  is located.

 2.   Steam  condensate  sprayed out  the  rear end of nozzle  when
     the  steam was turned  on.

 3.  The  carbon build-up in the  gooseneck  had a  tendency  to
    bridge over the  nozzle, thus  severely restricting the steam
     jet.

    The  first problem occurred  because  the return spring
operation resulted in impact stresses  that were  excessive.
A maximum of four Belleville washers were added  to the exist-
 ing rod  to reduce the impact.   This  number of washers proved
to be insufficient.

    It was determined that a modified design was  necessary to

                              161

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SELF CLEANING STEAM NOZZLES  (continued)

correct the problem.   The  rod  design was changed  so it could
accommodate additional washers.   An improved method of removing
condensate and reducing steam  blowback through the cylinder end
was provided by the addition of  a second piston  (Figure 52).
The push rod, upon being released,  will extend further into
the oven before retracting to  its normal position (1/16" past
the end of nozzle).   It was hoped that this additional
penetration of the rod would  help break up carbon formation.

    The  results  of this later modification  indicate  that
 steam leakage  past the piston rings  is  still  excessive, and
 this type  of construction is not suitable.

    An additional nozzle was made that extends an additional
1 1/2" into the standpipe.  For  over three months this nozzle
has not experienced a problem  with carbon build-up.   It has
been tried in two different ovens with no problems.   More of
these  nozzles will be tried.

    The present practice at P-4  battery is to manually ream out
each nozzle weekly.

Ascension  Pipe Elbow  Covers -

    Six designs   (Figure 53)    were built and tested on P-4
battery.  None of them achieved  any significant improvement
over the existing standpipe cap.  No further testing has been
attempted.

    The seating of the existing  caps was improved somewhat by
reducing the play between  the  elbow cover and the elbow cover
hinge  by inserting washers.  This causes the lid to close in a
repeatable pattern.   The present lid design will seal within 10
minutes at least 80%  of the time.  The present practice is to
wet seal when necessary after  the charge.  This consists of
pouring mud around the perimeter of the cap to seal all openings.

Charging Hole Lids

    This lid performance has been satisfactory.  One-quarter inch
was removed from the  lugs  to increase the clearance between the

                              162

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CHARGING HOLE LIDS  (continued)

lid lifter magnet and the top of the lid.  This  also  permitted
the lid to be oscillated in the charging hole ring without undue
interference with the lugs in the rings.

    The radial grooves in the lids permit positive  engagement
with the lid lifter magnet, so that the lids are assured of
rotating.  The lid lifter is able to properly  seat  the lids.

Oven Alignment

    The proper alignment of all battery mounted  equipment with
respect to the charging car was a necessary and  time  consuming
job. The following must be simultaneously considered  in making
a determination of the proper position:

1.  Car spotting panel is located to stop car  in the  desired
    position.

2.  Charging hole rings must be relocated so that the drop
    sleeve fit concentrically when lowered.

3.  The ascension pipe linkage of the oven to  be charged must
    be adjusted so that linkage levers and the steam  valve
    actuating mechanism are properly located when the actuating
    lever (#2) on the charging car is raised.

4.  The ascension pipe linkage of the oven that  is  to be pushed
    (two ovens south of the one being charged) must be in proper
    position so that when the actuating level  (#1)  on the
    charging car is lowered, the damper valve  closes  and the
    standpipe cap opens.

5.  The gooseneck locatdon of the oven to be pushed must be in
    the proper position so that the gooseneck  cleaner is able
    to enter and effectively clean the deposits  of  tar and
    char from within the gooseneck.

    Satisfying all these requirements simultaneously  was a
difficult task.  P-4 battery was placed in operation  in December
1953.   Batteries characteristically grow with  time, and the
original dimensions change non-uniformly.  This  dimensional

                             165

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Oven Alignment  (continued)

distortion required additional  efforts to ensure that alignment
tolerances were adequate  for  proper operation on this system.
Details of the dimensional  changes on the battery are given in
Appendix F.

    The general procedure followed in optimizing the car position
at a particular oven was  to free the existing charging hole rings
from the permanent brick.   The  car was then positioned for charg-
ing this oven by aligning the gooseneck cleaner drive tube and
flail with the center of  the  gooseneck inspection port.  Thus
the ideal reference point between the car and the battery was
at the gooseneck of an oven two spaces south of the one where
charging holes were to be relocated.  The larry car drop sleeves
were lowered so that the  charging hole rings could be concentric-
ally positioned.  Movement  of charging hole rings was limited
so that no constriction was made in the charging hole.  For
those few cases where a limit was reached,  the reference
position at the gooseneck cleaner was moved away from the ideal.
The car spotting panel was  then mounted so that the car would
always stop within _+ 0.35"  of this position.  The ascension
pipe linkage was adjusted for optimum operation.

Results -

    It was possible to relocate the charging hole rings on one
oven per day.  The occasional problem with drop sleeve seating
in #3 charging hole ring  is the result of not being able to
ideally locate the ring.  It  was usually necessary to re-
position the car spotting panel to achieve optimum spotting.
The ascension pipe linkages were then modified as necessary to
obtain satisfactory operation.   This consisted of bending the
linkages and adding extensions  to some.  On  some ovens
proper operation was never  consistently achieved because of the
interference between the  steam  linkages and the damper linkages,
and the wide variability  in critical dimensions.
                                166

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                          SECTION   ix

                   APPLICATION TO NEW BATTERIES
     The choice of charging equipment to be used on a new battery
 must be based on conditions that are expected to exist twenty
 years or more after it is placed in operation.  Consideration
 would be given to improving the environment of the personnel
 working on the battery top.  This would recognize the improvements
 of coking equipment that essentially result in smokeless charging,
 smokeless pushing, and minimal coke oven door leakage.  The
 success in achieving this improved environment depends to a great
 extent on the reliability of the equipment involved.

     Assuming the charging system utilizes a larry car, many of
 its operations would accordingly be mechanized.  The AISI/EPA
 concept of controlled oven gas pressure requires the use of a
 double gas off-take and a good steam aspirating system.

 CHARGING CAR

     The charging car would have most of the following features:

 1.  Enclosed operator's cab.
 2.  Environmental control unit.
 3.  Coal feed system.
 4.  Drop sleeves.
 5.  Lid lifters.
 6.  Ascension pipe damper mechanisms.
 7.  Gooseneck cleaner.
 8.  Coal bin gate operator.
 9.  Electric and hydraulic power.
10.  Automation.

 Enclosed Operators Cab

     The location of the cab on the charging car is an important
 operational factor.  It can be at the battery level  (LOW) or at
 an upper level  (HIGH) suitable for cleaning goosenecks.  The
 following table summarizes some of the features of either
 location.
                               167

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 Enclosed Operators Cab  (continued)

      Feature              High Level             Low Level

 Observe coal flow in           YES                    NO
 hoppers

 Inspect goosenecks             YES                    NO

 Clean goosenecks               YES               Only remotely
                                                 initiated mech-
                                                 anized  operation

 Observe charging          Only if suitable            YES
 conditions at             viewing system
 charging holes            provided  (mirrors)

 Easy access to equip-          NO                     YES
 ment near charging
 holes during charging
    The final  choice of the cab location will depend on  conditions
 at the local plant where the car will be operated.  The  high  level
 cab would  appear to be a safer environment for an operator.   If  a
 suitable viewing system can be provided, the HIGH level  location
 is preferred by this writer.

 Environmental. Control Unit

    An environmental control unit is an attractive  feature  for
 a larry car.   More work is needed to develop one that does  not
 require excessive maintenance and meets air quality standards.
 The worst  problem with the AISI/EPA larry car unit  is the large
 amount of  maintenance .required to keep it operative.  The
 improvement of the battery environment with smokeless charging
 and pushing, an minimal door leakage should significantly extend
 the life of the unit components.  A unit that will  filter out
particulates and regulate air temperature, requiring no  more  than
weekly maintenance,  would be a significant improvement.

 Coal Feed  System
    The simplest system that will provide a reliable feed is
                               168

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Coal Feed  System (continued)

preferred.  Gravity  feed  and  forced feed systems are available.
The requirements of  a  coal  feed  system have been discussed in
Section VIII  (page 105).  The type  of system that meets these
requirements best for  the conditions existing at a specific
battery should be selected.   Volumetric measuring sleeves should
be provided for  each hopper.

    A desirable  feature for a coal  feed system,  would be the
availability to  an operator of coal flow meters  for each hopper.
This operator's  tool would enable him to take immediate remedial
action when coal flow  is  not  proper.   A bottom level sensor is
almost essential.  It  would be used to close the hopper shut-off
valve and permit re-lidding.

Drop Sleeves

    Drop sleeves are required to guide the  coal  from the hopper
into the charging holes without spilling coal on the battery,
and seal the oven port.   The  type of  drop sleeve used depends on
the type of coal feed  system  and charging system used.   The
specific design must incorporate features that will not adversely
affect the coal flow from the hopper.

Lid Lifters

    Lid lifters are  a  very desirable  feature of  a charging
system.  They perform  a portion of  the work which otherwise
must be done by a Lidman.  When malfunctions occur that result
in flaming gases blowing  out  the charging holes,  the mechanized
operation permits instant re-lidding.   Careful consideration
must be given to heat  sensitive components  in seeing that they
are properly protected.

Ascension  Pipe Damper  Mechanisms

    A mechanized ascension pipe linkage operator that can be
initiated by a push button to  place an oven on-the-main,  or
damper-off, is a very useful  operating tool,  if  it is reliable.
The present performance of the mechanisms at P-4 battery has not
reached an acceptable  level of reliability  as indicated in
Section VIII,  page 116.   The  reliability has not been attained

                               169

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Ascension Pipe  Damper Mechanisms (continued)

because  the design  does not yet satisfy all the necessary
operating conditions.   The design of such a linkage on a new
battery  could be  improved as a result of known problems that
occurred at P-4.  It  is believed that a reliable system can be
designed and built.   The improved operating and working
conditions that can result from the use of mechanized ascension
pipe linkages suggests that enough work should be done in this
area to  assure  that reliable operation is achieved.

Gooseneck Cleaner

    A mechanized  gooseneck cleaner is a desirable operating tool
that has been furnished on recent larry cars.  The operating
controls for these  mechanisms have been at the gooseneck cleaner
itself.   The gooseneck cleaner for the AISI larry car went one
step further by making provision for self alignment so that it
could be operated remotely from within the cab.  The self-
aligning design has not yet been field tested, so that its
reliability is  not  proven.

    A mechanized  cleaner will promote more regular cleaning of
goosenecks and  as such is a recommended feature on a new larry
car.  Its location  on the larry car must be planned to minimize
the larry car operating cycle, such as using it on an oven
different from  the  one being charged, if the charging sequence
will permit

Coal Bin Gate Operator

    A power operated  coal bin gate operator is recommended for
a new larry car.

Electric and Hydraulic Power

    Electric power  is  required for all cars.  Most recent cars
have utilized 460 volt a-c three-phase power.  250 volt d-c power
was provided for  most  older cars and a few recent ones.  The
selection of the  power supply is often a function of availability
at the local plant  level.  Some plants prefer d-c power since
constant potential  control for traction drives are less complex
and require less  technical "know-how" to maintain.
                              170

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Electric and Hydraulic Power  (continued)

    This writer believes that most new batteries  will  prefer the
use of 460 VAC because:

1.  It is usually more readily available.
2.  Many functions utilize standard a-c motors.
3.  Less difficulty in minimizing ground loops by ease of  isola-
    tion.
4.  Many electric and control devices more  readily available in
    a-c.
5.  Commercial a-c to d-c power conversion  equipment is readily
    available where needed.

    The use of stainless steel power supply rails are  preferred
because of less deterioration from the battery environment and
improved contact at the collector shoe as a result of  less
corrosion.

    Some of the larry car functions can be  better performed by
hydraulic power, and consequently a hydraulic system is recommend-
ed.  The experience with the AlSIcar indicates that sufficient
reliability can be built into the system for practical usage.
Where improved operating performance of sub-systems can be
attained by the use of hydraulics, the equipment  should be
carefully selected.

Automation Hardware

    Most of the equipment provided on a larry car will require
some measure of automatic sequencing.  The  type of control
equipment used external to an enclosed cab  and control room
must be selected with extreme care.  Failure of sensors was a
severe problem on the AISI/EPA larry car.   They are exposed to
the full range of environmental conditions  from oven flames to
quench tower sleet.  The number of sensors  used should be minimal,
limited to only those necessary to reliably sequence the
equipment.  Consideration should be given to using on  certain
applicable functions, hydraulic pressure switches that can be
located in an enclosed cabinet.  Sensors that are required must
be suited to the conditions to which they are exposed.
                              171

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Automation Hardware  (continued)

    The sequencing control  can  utilize either mechanical relay
logic or static logic.   Static  logic was originally selected
for the AISI/EPA larry car  because  of the necessity to get
all the equipment in the available  space.  Relays were used
only to perform the necessary final output functions.   An
environmentally controlled  atmosphere was available.   The
logic equipment has performed reliably.

    Several factors to be considered in making a selection of
sequencing control equipment are  as follows:

1.  Reliability
    Static logic, properly  applied  and installed will  be more
    reliable.  Most installations have relays for the  final out-
    put.  This is no longer a necessity since direct  static
    switches such as Triacs are available.

2.  Flexibility
    Changes to the control  sequence can be made much more
    readily with static  logic than  with relays.  If no  new
    sensors or outputs are  involved,  it usually involves only
    minor changes in the backplane  wiring.  Spare logic
    elements are more readily available.   Wiring changes to
    relays are more difficult to  make .

3.  Trouble Shooting
    An experienced technician can probably trouble-shoot static
    logic, furnished with status  indicating lights, using a volt-
    ohmmeter in the same time span  or less as that involving
    relays.  Where experienced  technicians are not available on
    a 24-hour basis, the use of relays  would  be favored.  If
    the control sequencing  is relatively  complex,  then static
    logic is favored if technicians are  available.

4.  Environment
    The coke oven environment favors  the  use  of relays unless
    controlled conditions are assured.   There have been no
    observed problems with  the  logic  on  the AISI/EPA larry car
    that are related to the environment.   If  an environmental
    control unit is furnished on  the  car,  there would  be no
    need to rule out the use of logic equipment
                             172

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Automation  Hardware  (continued)

    The use of relay  logic would  be preferred in most coke plants
because of  trouble shooting  difficulties with untrained personnel
and the inability  to  continuously maintain an controlled environment

Automatic Sequencing

    The automatic  sequencing of  individual operations initiated
by the larryman is preferred.  These operations would include:

1.  Normal  car travel - master switch.
2.  Unidirection creep travel for gun sight spotting by push-
    button.
3.  Emergency travel by pushbutton causing all  equipment to move
    to travel position.
4.  Remove or replace lids.
5.  Place oven on-the-main.
6.  Damper off on oven.
7.  Start and stop coal feed  (automatic  stop when empty)
8.  Clean gooseneck.
9.  Coal bin gate operator.

A voice system between the pusher machine  and larry  car is
necessary for coordination.

    The use of an automatic  system utilizing control signals
between the pusher machine and larry car is not necessary (refer
to Section VIII,  page 140).  A pusher machine - larry  car
alignment interlock,  although useful, is not necessary.

PUSHER MACHINE

    The worst case leveler bar duty cycle  should be  determined
so that its design and material will satisfy the operating
conditions.  The automated motion of the leveler bar is recommend-
ed.  This sequence would include  a definite number of  strokes dur-
ing the final pass to assure a clear gas passage in  the oven
after charging.

    A smoke seal must be provided that minimizes any opening
around the leveler door.  During  operation of the leveler bar it
must continuously maintain a  tight fit between  the leveler door

                              173

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 PUSHER MACHINE (continued)

 opening and the smoke seal, as well as between  the  smoke seal
 and the leveler bar.  A mechanized leveler door operator is
 desirable.
 CONSIDERATIONS ON THE BATTERY

 Double Gas Off-Take

    A double gas off-take would be achieved on most  new batteries
 by the selection of a double collecting main.  If  the  experience
 in using jumper pipes from an extra smoke hole shows comparable
 overall results at less maintenance, then this approach can  be
 considered.

 Adequate Steam Aspirating System

    An adequate steam aspiration system is required  to direct all
 the gases generated or displaced during charging into  the collect-
 ing main.  The experience with the 693 ft3 ovens at  P-4 battery
 indicates satisfactory aspiration is obtained with 120 psi steam
 pressure applied to a 3/4" steam nozzle on a design  "A" gooseneck
 (Figure 51),  with a jumper pipe arrangement shown on Figure  31.
 This configuration provides a gas flow of approximately 1300 SCFM
 at each ascension pipe.  Part of the gas flow in the second
 ascension pipe originates in the adjacent oven.

    A steam supply pressure reducing control that permits
 adjustment of the steam pressure is desirable to limit the steam
 usage to only that amount required.  The steam piping to individual
 ovens must be of sufficient size to assure adequate  pressure at
 the steam nozzle.  Two steam supply lines to a 4" header were
 provided at  P-4 battery to assure adequate pressure  at all ovens.

 Operation of Ascension Pipe Mechanisms

    The design of the gooseneck cleaner, damper, steam, and  lid
mechanisms must incorporate provisions to assure proper operation
with the  dimensional position variations that can be expected
during the life of a battery.  These considerations  involve:

                            174

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Operation of Ascension PifeeMechanisms  (continued)

1.  Overall battery growth.
2.  Change in standpipe position because of difference in the
    collecting main movement and battery growth.
3.  Change in larry car Position resulting from rail movement
    as well as normal car positioning errors.

    To a lesser extent these considerations apply to the drop
sleeve which,  depending on the design, may have to seat within
the charging hole ring.
                              175

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                            SECTION X

                APPLICATION TO EXISTING BATTERIES

    The modification  of  an existing battery to achieve "smokeless"
charging must be done with due consideration to its present operat-
ing condition.  As  a  result of the experience gained in mechanizing
the operation at P-4  battery,  it is recommended that the scope of
work involve no more  than required to meet necessary goals in
eliminating charging  emissions.

DOUBLE GAS OFF-TAKE

    The first consideration is to determine the method of obtain-
ing a double gas off-take.  Many existing batteries have a double
gas collecting main which fulfills this requirement.  For the
remainder of the batteries having single collecting mains, some
modification will be  required.  If a battery was furnished with
an extra smoke hole (such as P-4 battery),  then the use of jumper
pipes provides a good solution.

    The remaining batteries with single gas collecting mains having
no spare smoke hole require special study.   Among some possible
considerations to be  investigated are:

1.  Addition of smoke hole at  each oven so that either jumper pipes
    or a second gas collecting main could be installed.

2.  Use of a jumper pipe attached to the larry car to connect
    one charging hole with a similar one on an adjacent oven.

ADDITION OF SMOKE HOLE

    Most ovens can  be modified to incorporate a smoke hole.  There
are a few oven designs.that would make this job difficult.  The
age and condition of  the battery would be an important consideration

    It would probably take 80-90 working days to build smoke holes
into an 80 oven battery.   This is based on a required time of seven
working days per oven as follows:

                             176

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ADDITION OF SMOKE HOLE  (continued)

             Days                      Task
              2                Cool down
              1                Tear out brick
              2                Rebuild
              2                Heat-up and do hot work

Ovens would generally be taken out of service in groups of six or
eight.

    The rough estimated costs on a per-oven basis are:

                   Labor                  $3,000
                   Material                  500
                   Engr.,  Supv.,  Overhead    500
                   Total                  $4,000
                   80-oven battery      $320,000
ADJACENT CHARGING HOLES

    This modification has been reported in operation at several
                              176a

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 ADJACENT  CHARGING HOLES (continued)

         3,  5,  15   _   .
 batteries.            The jumper pipe is carried  and  set  in
 place by  the  larry car.  The end charging hole at  the  opposite
 side from the collecting main is generally used.   A  typical
 procedure is  to  charge that port first, then open  the  valve  to
 the jumper pipe  and use it  for the second gas off-take.   One
 installation  charges with #1, 2 and 4 hopper only  and  uses the
 jumper  pipe at #3 charging  hole.15

    Reported  problems with  these methods involve:

 1.  Impscper seal  between charging hole and jumper pipe.
 2.  Must  perform frequent cleaning of the jumper pipe.
 3.  More  work for the lidman.

 ADEQUATE  STEAM ASPIRATION

    Many  existing batteries will not have sufficient steam
 aspiration.   A first consideration is to utilize the available
 steam.  Since there are so  many variables which determine the
 required  steam ejection,  the best approach is to make  actual
 tests on  a pair  of ovens.   Factors such as oven size and
 ascension pipe dimensions and configuration affect the required
 aspiration, which determines the general steam requirements.
 From known characteristics  of similar type ovens, or extrapolating
 the results of published data, an approximate level of gas flow
 is determined.   In the absence of any available data,  the gas
 flow for  any  particular ascension pipe arrangement may be measured
 using the EMPTY  OVEN TEST procedure described in Appendix E.   A
knowledge of  the existing aspiration characteristic as shown on
 Figure  51 (pg. 159) can be  used to estimate the  new  requirements.

    Aside from data given in this report, steam aspirating
 requirements  for existing batteries are available  in many
 published papers.3'  ^-'       It is interesting to  note that
measurements  of  an average  gas evolution  of 4000  SCFM during
 the first two minutes of charging a 1391 ft3 oven  are  not quite
double  our estimated requirements  (pg. 174) of about  2200  SCFM*
 capacity  for  a 693 ft3 oven.

   * 2600 SCFM  total with  an estimated 400 SCFM from
     the adjacent.oven.

                             177

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ADEQUATE STEAM ASPIRATION  (continued)

    Using equations contained  in Appendix E  and curve character-
istics similar to those of Figure 51,  the new steam requirements
can be estimated using the characteristics  of the  available steam
pressure temperature, and nozzle configuration.

    Based on the estimated steam and nozzle requirements,set up
a temporary steam line to a pair of ovens and observe the
results during actual charging conditions.   If the second gas
off-take cannot be made available for  this  test, then provide
sufficient capacity for smokeless charging  during  the first
75% of the charge (prior to blocking the  gas passage at the
top of the oven)  from one ascension pipe.

    The required steam may be calculated  once the  requirements
on an oven have been determined.  A steam pressure regulating
station is recommended so that optimum steam pressure may be
determined after the installation is complete.

LARRY CAR REQUIREMENTS

    Since existing batteries have a larry car/ the first consid-
eration is to make necessary modifications  as required, provided
the car is in satisfactory condition.  The  AISI/EPA charging
system requirements that affect the larry car are:

1.  Sealed oven ports
2.  Controlled coal feed system
3.  Sequential relidding of oven ports

    Most existing cars have some type  of  drop sleeve,  but in some
cases they are all operated from one mechanism.  The drop sleeves
must be individually operated to permit sequential relidding.

    The fit of the drop sleeve with the charging hole ring must
be sufficient to form a seal.  Some method  is required to seal
the drop sleeve open port after charging.   A bottom coal level
sensor can be provided to stop the coal feed at the proper time
and initiate any sequence necessary to seal the port.

    A coal seal may not be convenient  to  use on many cars.

                              178

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LARRY CAR REQUIREMENTS  (continued)

Some existing table feeder larry  cars  are being modified by
using a cylindrical plug in the gas  exhaust stack above the drop
sleeve.  This plug is lowered  to  seal  the opening from the drop
sleeve to the hopper when the  level  detector stops the coal feed.
A slide gate arrangement can be used on some gravity feed cars.

   The requirements for controlled  feed are satisfied by
individual hopper feed  control and coal level sensors.  Gravity
feed or forced feed larry cars may be  used.  Volumetric measur-
ing sleeves are necessary to assure  each hopper of a consistent
coal charge volume.

   Sequential lidding  of oven ports can still be done by the
lidman.  Some operators may wish  to  add automatic lid lifters
to relieve the lidman of this  task.  The addition of lid lifters,
although desirable, may be difficult,  depending on the condition
and design of the existing car.

PUSHER MACHINE MODIFICATIONS

   Assuming the existing leveler bar  is designed to handle the
required duty cycle, provision should  be made for a smoke boot
to seal the leveler door opening.
                              179

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                           SECTION XI

                            COST DATA

CAPITAL COSTS

    The capital costs of the system  installed  at P-4 battery have
been estimated by eliminating the abnormal  costs of the  total
project which includes considerable  development work.  The break-
down in subparts is an estimate based  primarily on information
supplied by Koppers.  Cost data represents  1970-1972 levels.

    The costs of the larry car are shown  in Table 10.  Table 13
shows some automatic features that were furnished with this
prototype system, that would not usually  be included.  Table 11
shows the costs of modifying the pusher machine,  assuming the
existing leveler bar can be used.  Table  12 shows the costs of
modifying the battery. Table 14 contains estimated costs  of a
new leveler bar.
INSTALLATION

    The lost production during installation was very small since
the larry car was installed at the extreme  south end of  the
battery.  The alignment of charging  hole  rings  and the placement
of the car positioning panels was performed for the most  part
with about 4 to 6 hours charging delay per  oven.
                             180

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                           Table 1O.   LARRY CAR CAPITAL COSTS

                                   (1970-1972 dollars)
Component
Frame
Traction drive
Lid lifters
Damper and steam
operator
Ascension pipe
cleaner
Peed hoppers
Butterfly valves
Level sensors
Bin gate operator
Hydraulic system
Butterfly hydraulicc
Environmental equip-
ment
Miscellaneous Elec .
and supply
Voice communication
system
Electric checkout
Total
Material
Costs
$80,536
48,345
72,334
11,681

7,753

18,650
23,850
5,134
8,832
24,308
19,800
23,607

44,369

3,529

—
$392,728
Engineering
Costs
$38,298
12,469
14,321
3,211

29,062

11,869
19,464
5,855
8,544
6,050
5,000
5,284

4,620

5,299

—
$169,346
Installation
Labor
$16,516
8,999
19,624
12,374

8,000a

7,422
3,859
4,240
4,880
5,826
4,720
2,130

15,500

2,000

22,000
$138,090
Total
$135,350
69,813
106,279
27,266

44,815

37,941
47,173
15,229b
22,256
36,184
29,520
31,021

64,489

10,828

22,000
$700,164
00
H1
        a.   This  anticipates labor costs.
        b.   Costs of using latest level sensor would  probably be  less  than 50% this
            value.
        c.   This  is  cost of that part of the hydraulic  system required for the
            butterfly valve type of gravity  coal  feed.
        d.   This  includes a-c supply and collector  rail system on existing collector
            supports. The installation labor for this  item does  not include
            supervision.

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         Table 11.  PUSHER MACHINE  CAPITAL  COSTS
                    (1970-1972 dollars)
Component
Leveler bar
relocation
Leveler door
oper.on 79 doors
Leveler bar seal3
Total
Material
Costs
$2,500
75,268
23,420
$101,188
Engineering
Costs
$10,388
27,058
11,314
$48,760
Installation
Lab or c
$13,546
7,761
9,193
$30,500
Total
$26,434
110,087
43,927
$180,448b
a.  This mechanism includes a coal chute.




b.  This does not include a new leveler bar, if required,




c.  Installation labor does not include  supervision.
                          182

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      Table 12.  BATTERY MODIFICATION CAPITAL COSTS

                   (1970-1972 dollars)
Component
Steam aspiration3
Self cleaning
steam nozzles
Ascension pipe damper
lid & steam linkages
Jumper pipes
Charging hole lids
Battery reinforcing6
Total
Material
Costs
$25,284
7,290
/
30,000
80,000
8,698
10,000
$161,272
Engineering
Costs
$3,080
2,215
4,000
5,000
585
2,500
$17,380
Installation
Labor f
$17,428
3,000
14,000
40,000C
323
6,500
$81,251
Total
$45,792
12,505
48,000
125,000
9,606
19,000d
$259,903
a.  Includes new steam supply lines,  header,  pressure regulator,
    piping to individual ovens,  steam valves.

b.  Self-cleaning steam  nozzles have not yet been proven
    successful.

c.  Anticipated  labor costs.

d.  Does  not include reinforcement of collector rails.

e.  Reinforce south end battery, remove coal  bin scale
    and replace  with steel stools, install hydraulic
    car bumper at south-end of battery.

f.  Installation labor does not include supervision.
                           183

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            Table 13.  CHARGING SYSTEM OPTIONS
                    (1970-1972 dollars)
Component
Larry car
position system
UHF alignment
system
Current signal
system
Automatic charging
mode
Total
Material
Costs
$12,678

15,681
41,163C
50,000e
$119,522
Engineering
Costs
$12,344a

2,215
6,643

$21,202
Installation
Labor
$20,537b

2,000
16,567d

$39,104
Total
$45,559

19,896
64,373
50,000
$179,828
a.  Engineering costs include structural study and determina-
    tion of proper reinforcement of collector rail supports.

b.  Includes cost of reinforcing collector rail supports
    (about 60% of installation labor).

c.  Includes control equipment in larry car, pusher machine,
    battery, and wayside loops.

d.  Primarily cost of installing wayside loops.

e.  Logic control equipment in larry car.

f.  Installation labor does not include supervision.
                           184

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                 Table  14.   LEVELER BAR COSTS
    Component
  Material
 Vendor
Quotation
Standard  leveler bar
Wedge  type  leveler
bar
A-36 steelb
A-517-68 Gr.Jc
A-36 steel
A-517-68 Gr.J
 $6,700
  8,800
  8,600
 11,800
    a.   Quotations  to  Koppers,  January   1974
    b.   Standard  type  steel used on existing bar
    c.   Recommended type steel
                             185

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OPERATING AND MAINTENANCE COSTS

    An evaluation of projected operating and maintenance costs
related to the new charging system at P-4 battery  is based on
a comparison of the qualitive change of cost elements.

ENERGY REQUIREMENTS

    The required aspirating steam at two ovens per charge increases
the estimated steam requirements by a factor of 4.7.  This increase
corresponds to a steam usage of 6100 Ib/hr. during charging.
Based on five minutes/charge and five charges/hour, the steam
requirements, neglecting leakage, are 2540 Ib/hr.

    The larry car has the following estimated electrical
requirements.
    Charging (Cycle pump loading)                30-60 KVA
                             estimated average   40 KVA
    Traction Drive           accelerate          120 KVA
                             steady state        30-40 KVA
    Car Idle (Environmental control unit)        5-10 KVA

OPERATING PERSONNEL

    There has been no change in the manpower requirements to
operate this battery.  Three operators are required to charge
coal in the ovens.
               1)  charging car operator
               2)  pusherman
               3)  lidman

MAINTENANCE PERSONNEL

    The required maintenance on the larry car is shown on Table
15.  Additional maintenance requirements related to charging are
shown on Table 16.  The estimated maintenance requirements are
base d on data taken over a three month period  (December 1973 -
February, 1974).  The estimated requirements account  for the fact
that the car was in use slightly less than half the time and
also reflect expected improved performance of hydraulic equipment.
The estimated 79 manhours per week of millwright,  oiler, and
electrician maintenance service is believed to be  double the
previous repair work used on the P-3 larry car.  The maintenance
                                186

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       Table 15.  LARRY CAR MAINTENANCE REQUIREMENTS
Component
Hydraulic system
Main hydraulic unit
Hydraulic leaks
Hydraulic hoses
Mechanical equipment
Lubrication
Environmental control
unit
Change throw- away
filter
Clean Louvers, change
bag filter
General maintenance
Electrical system
Clean equipment,
check filters, check
for grounds
Replace damaged equip.

Craft3
Millwright
Millwright
Oiler
Millwright

Electrician

Weekly Maintenance Man-hour
Requirements
Preventative
'Maintenance
2
4
4
10
3
10
13

2
2
2
6
6
6
41
Breakdown
Repairs
4
4
8
6
6


0
8
22
a.   Millwrights  work in pairs - break-down hours are 1/2
    man-hour.  Electrician usually works singly - break-down
    hours  equal  man-hour.
                          187

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        Table 16.  OTHER CHARGING MAINTENANCE REQUIREMENTS
       Component
  Craft
   Repair and
Maintenance
Pusher machine
 Door opener
 Leveler bar, smoke shield
 Electrical
Ascension pipes
 Damper - lubricate
 Damper and lid linkages
 Steam linkages
Jumper pipes (weekly clean-out)
Millwright
Millwright
Electrician
Oiler
Millwright
Millwright
Lidman
   3
   1
   2
   2
   4
   4
           16

           14
           30
                             188

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MAINTENANCE PERSONNEL  (continued)

requirements have increased 40 man-hours.   This does not include
estimates for increased supervision.   The  greater complexity
of the hydraulic and electrical  systems  necessitate the availability
of qualified supervisory personnel.   The increased supervision
time is in the range of 12-16 man-hours  per week divided equally
between electrical and mechanical-hydraulic.

   The efficient operation of this battery,as related to the
present practices of Pittsburgh  Works, requires that equipment
be available for satisfactory production use about 95% of the
scheduled time.  This assumes a  given piece of production apparatus
will be scheduled for eight hours maintenance per week and that
for the remaining 20 turns, it will be available for operation
152 hours.

   The data in Table 15 indicates that  the scheduled maintenance
can be done in eight hours with  an average of two millwrights and
1 1/2 electricians.  The average breakdown time is almost 16
hours which corresponds to 90% availability of the larry car.

   The future addition of jumper pipes  and improved reliability
in the coal feed system are expected  to  improve the car reliability.
The average larry car availability under these conditions is
expected to be about .95%.
                              189

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                          SECTION XII
    Dancy, T. E.
    Wilputte, Louis N.
    and Wethy, Frans
3.  Meads, M. R. and
    Randall, G. E. C0

4.  Still, Firma Carl
    Dukhan, V. N.
6.  Varshavski, Denisov,
    Zlatin, and Zolotarev

7.  The British Coke
    Research Association
8.  Barnes, Hoffman, and
    Lovmie, Battelle
    Memorial Institute
    Connolly, J. p.
BIBLIOGRAPHY

  "Control of Coke Oven Emissions",
  American Iron and Steel Institute,
  May 27,  1970.

  "Recent  Improvements to Coke Oven
  Design and Operation",  Blast Furnace
  and Steel Plant, 34, March,  1946,
  Pages  355-367.

  "Smokeless Charging", Coke Oven
  Managers Association Proceedings (1961).

  Recklinghausen,  Germany, "Method and
  Apparatus for Charging Material Into
  a  Coking Furnace Unit", U.S. Patent
  3,623,959, November 30, 1971.

  "Developing Methods of Smokeless Coke
  Oven Charging",  Coke and Chemistry
  U.S.S.R. #7,  1963 Pages 25-30.

  "Smokeless Charging of Coke Ovens",
  Coke and Chemistry U.S.S.R. #6  , 1965.

  "Practical Suggestions for the
  Reduction of the Emission of Smoke,
  Dust,  and Grit at Coke Ovens",
  Special  Publication 5,  September 1969.

  "Evaluation of Process Alternatives  to
  Improve  Control of Air Pollution from
  Production of Coke" for National Air
  Pollution Control Administration,
  Department of Health, Education, and
  Welfare, January 31, 1970.

  "Report  on Ascension Pipe Steam Ejector
  Test Program",  AISI, September, 1970.
   (restricted  distribution)
    190

-------
BIBLIOGRAPHY (continued)

10.  Plaks, Norman
11.  McCord, J. C.
12.  Stoltz, J. H. and
    Lee, J. R.
13.  Edgar, W. D. and
    Muller, J. M.

14.  Weber, G. T. and
    Lewis, R. E.

15.  Mautz, G. H.
"Improved Processing Methods  for  Control
of Air Pollution Emissions  from Coke-
making", Presented at  the Economic
Commission for Europe  Seminar;  Leningrad,
U.S.S.R. 1971.

Lackawanna's Experience Operating No.9
Coke Oven Battery, Iron Making  Proceed-
ings, Volume 30, 1971.  Page  94.

"AISI Coal Charging System, Progress
Report 2", Ironmaking  Proceedings,
Volume 31, 1972, Page 249.

"The Status of Coke Oven Pollution
Control", AIME Conference,  April,1973.

"Stage Charging", AIME Conference,
April, 1973.

"Three Hole Charging on a Four  Hole
Battery", AIME  onference,  April, 1973.
                               191

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                           SECTION XIII

                            GLOSSARY

Charge Cycle Time - Time  interval from  start of coal charge (first
    butterfly valve opens)  till  re-lidding complete (all charging
    hole lids in place).

Charging On-The-Main -  Opening the  damper  valve to connect an
    oven with the gas collecting main through an ascension pipe,
    and with fluid ejectors turned  on to draw charging emissions
    into the collecting main.

Charge Time - Time interval from start  of  coal charge till final
    coal feed (last butterfly valve closed).

Oven Ports - Oven openings  consisting of the charging holes, leveler
    door, and the ascension pipe elbow  cover.

TO -  Number of seconds of  no smoke during charging.

TI -  Number of seconds in which smoke  opacity is less than 20%
      (Ringelmann #1),  but greater  than TQ.

^2 -  Number of seconds in which smoke  opacity is less than 40%
      (Ringelmann #2) but greater than  Tj.

T.J -  Number of seconds in which smoke  opacity is equal or greater
—    than 40%  (Ringelmann #2)

PB -  Pushbutton
Smokeless Charging - Any and  all  emissions from oven ports less
      than 20% opacity during the entire charge cycle time.
      Opacity readings are determined  at the source.
                              192

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GLOSSARY (continued)

w.c.. - Water column - a measure  of  relative gas pressure in terms
      of a differential water column heighth in a U-tube manometer
      referenced to atmospheric pressure.
                              193

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                           SECTION XIV

                        CONVERSION FACTORS

    Environmental Protection Agency policy  is  to  express all
measurements in agency documents in metric  units.  When imple-
menting this practice will result in undue  cost or lack of
clarity, conversion factors are provided for the  non-metric units
used in a report.  Generally, this report uses British units of
measure.  For conversion to the metric system, use the following
conversions:
To Convert from

Btu/lb-F
Btu/min
Btu/ton
cfm
OF
ft
gal.
gpm
hp
in. we
Ib
lb/ft3
oz
psig
  To
J/kg-C
  W
j/kg
m /sec
  °C
  m
  1
I/sec
  W
N/m2
  kg
kg/m3
N/m2
N/m2
Multiply by

4184.
17.573
2324.444
.0004719
5/9  (°F-32)
.3048
3.785
0.0631
745.7
248.84
0.454
16.018
430.922
6,894.757
                               194

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                      SECTION XV





                      APPENDICES
A.  Oven Pressure Measurements                  196




B.  Reliability Data                            198




C.  Leveler Bar Investigation                   213




D.  Emission Data                               250




E.  Empty Oven Tests                            272




F.  Battery Dimensional Variations              280




G.  Ascension Pipe Particulate Sampling         284
                         195

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                            APPENDIX  A

                    OVEN PRESSURE MEASUREMENTS

    Measurements of the oven pressure  during charging were  made
at the smoke hole  (located on coke  side  of oven - Figure 1) by
J. R. Lee.  A pressure recorder was mounted on the larry car,
and pressure tubing was connected to a test lid with a small hole
drilled in the center.  The test lid was placed on the smoke hole
and sealed with asbestos rope and mud.   The pressure in the oven
at the smoke hole was then recorded throughout the charge.  Eight
pressure recordings were made from May 25,  1973 to June 15, 1973.
The results verify that the efforts to prevent blockage of  the gas
passage have not been adequate.  In every charge the pressure
increased significantly when the leveler bar was used during the
coal feed.  The maximum pressure at the  smoke box during leveling
averaged 8.5 inches of water column  (max.  - maximum 13 inches,
min-maximum 3 inches).  This compares  with an average maximum
pressure of 1 inch of water column  (max.  - maximum 4 inches, min-
maximum 1/2 inches) during the 75%  charge prior to leveling.

    Also observed in these tests, is that the longer that the 1st
75% of the coal charge is leveled before the final 25% is started,
the longer it takes for the coal blockage in the gas passage to
occur.
Date
5/31/73
6/31/73
5/30/73
5/25/73
5/31/73
5/31/73
5/31/73
5/31/73
Oven
No.
2-17
2-17
2-24
3-3
2-19
2-15
2-15
2-21
Duration of Leveling
Before Final 25%
4
12
15
33
34
45
45
180
seconds
seconds
seconds
seconds
seconds
seconds
seconds
seconds
Time Until 1st Coal
Blockage
0
0
12
15
16
12
18
21
seconds
seconds
seconds
seconds
seconds
seconds
seconds
seconds
    A copy of a pressure recording  taken  on oven 2-19 on 5/31/73
is shown on Figure  54.
                               196

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                                             5/31/73
                                              LEVEL,
                                       PASTS STARTS * - -
IS   36  54   72  90  108  126  [44  162  180 138 216  234- 252 270 Z8B 306 324

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                           APPENDIX  B

                   LARRY CAR  RELIABILITY DATA
CRITERIA

    The criteria used to determine minimum acceptable  larry car
performance are:

1.  The car and associated charging equipment  are  available for
    satisfactory production operation 90% of the total operating
    time.

2.  The required scheduled maintenance shall not exceed a  total
    of eight hours during any one week period.

LARRY CAR AVAILABILITY

    The quantitative evaluation of this criteria in  terms  of
larry car availability is determined from the  following relation,
defined in Figure 55.
                 =  P  x  100                           (1)


    This measure of larry car reliability is essentially the ratio
of actual charging time to the total scheduled  time  that the
car could be used for production charging.  The difference between
"p" and "n" represents the normal time required for  making break-
down repairs and the extra maintenance requirements  that exceed
the 8 hour/week rate.

OPERATING PROBLEMS

    The available charging time "n" does not include lack  of
production use because of operating problems not associated directly
with the car reliability.

    The nature of the operating problems which prevent the use of
the new larry car during charging can best be  understood by
referring to Figure 57 (page 206);  which shows  the  location of the coal
and the larry cars used at P-4 battery.  When  the  new  P-5  larry  car
is used to charge ovens on P-4 battery, the old spare  P-4  larry

                               198

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OPERATING PROBLEMS  (continued)

car is parked at the center of  the coal bin.  The P-3 larry car
then uses the north side of the coal bin to get coal for charging
p-3 battery, and the P-5 larry  car uses the south end of the coal
bin to get coal for charging  P-4 battery.

   If P-3 larry car breaks down and requires repairs it must be
parked in the center of the coal bin.   It  is then necessary to use
P-2 larry car to charge P-3 battery and P-4 larry car to charge
P-4 battery.  Under these  conditions,  which will not exist when
P-4 car is dismantled, it  is  necessary to  take P-5 car out of
service.

   Another temporary operating condition  which requires taking
the P-5 car out of service occurs when the south end of the coal
bin is empty and it becomes necessary  to get coal near the center.
It is then necessary to use P-4 car to charge ovens on P-4 battery.

   Occasionally P-5 car is not used if a trained operator is not
available to run the car on any particular turn.  This usually
occurs if the regular operator  reports-off sick, and the back-up
man does not have sufficient  training.

   It has become necessary to  clean  the goosenecks and return
bends of the gas off-takes on a weekly basis over and above that
done by the operator during charging.   The man doing the cleaning
stands on a platform so that  he can use a  bar to clean out through
the ascension pipe inspection port.   The clearance between this
platform and the new P-5 larry  car is  very small (less than 1")
while that with the P-4 car is  almost  12".  Consequently when
this work is performed, the spare P-4  larry car is used for charg-
ing in order to realize the necessary  safety condition for a man
performing the cleaning.  This  procedure should not be necessary
when the mechanized gooseneck cleaner  is operational.

AVAILABLE PRODUCTION CHARGING TIME

   The available time for production  charging with the new P-5
larry car is defined in Figure  55 as

                n = t- (b+m1+mp+f  + w2) .       (2)

                               199

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      Definition of Larry Car Availability  and Utilization

       A = -5- x 100                                    (1)
       n = t -  (b + m1+mp + f+ w2)

       p = n -  (r + m2  + w.^)                             (3)
       U = -"- x 100                                    (4)

where  A = larry car availability  for production  operation,
           per cent
       p = actual time used  for production  charging,  hours.
       n = available time for production  charging with  this
           larry car, hours.
       t = total scheduled time for  charging  P-4  battery
            (normally 24 hours/day),  hours.

       b = time not available for  charging  with this  larry car
           because of operating problems  not  associated with
           this charging system reliability,  hours.
      mi = time utilized for scheduled maintenance that is less
           or equal to a limit of  8  hours/week, hours.


      m2 = maintenance time utilized which  exceeded the allowable
           8 hours/week scheduled  maintenance, hours.

      nip = time utilized to perform  design  modification work on
           the larry car, hours.

       f - time the car is not used  for production charging, but
           is in operating condition.  This is specifically the
           elapsed time from completion of  repair work until the
           larry car is placed in  service,  hours.

      w-^ = normal time' waiting for repair craft to start  repair
           work, hours.  This assumes no  other larry  car  is avail.
           able to charge P-4 battery.
                             Figure 55

                              200

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Definition of Larry Car Availability and Utilization

                      (continued)

v?2 = time waiting for repair craft to start repair work,
     hours.  This assumes that a spare car is available
     and the craft delay repair work because there are
     higher priority tasks to be completed first.

r  = actual time required for repairs, hours.

U  = larry car utilization, per cent.  This represents
     the time available to charge with the new larry car
     compared with the total time period.
                     Figure  55

                         201

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AVAILABLE PRODUCTION CHARGING  TIME (continued)

    In addition to the unavailable time because of operating
problems, b, maintenance time  that is either within the maximum
8 hour/week rate or that is of a  project nature,  such as design
modifications, is also excluded.

    Two other factors are  recognized  that relate to the availability
of the spare P-4 larry car.  If a failure occurs with the new P-5
car, it is parked at the south end of P-4 battery for repairs and
the spare car is used for  charging.   Since no production is being
lost, the required repair  personnel may work on more pressing
repairs elsewhere that may be  affecting production.  The resulting
interval, W2, between the  time of failure and the time repair
work starts, is not included as part  of "n".

    After completion of repair work,  it may not be convenient
to remove the spare car from production charging and place the
new car in service.  This  elapsed time,  f,  occurs only because
there is a spare car, and  is not  considered as  part of "n".

ACTUAL PRODUCTION CHARGING TIME

    The actual production  charging time "p" differs from the avail-
able charging time "n" as  given by the relation in Figure 55.

             P = n-(r+m2+w1)                      (3)

    The normal delay time, w-j_,  represents a delay in starting
repair work because the required  craft is not immediately
available under the assumption of no  spare larry car.

LARRY CAR UTILIZATION

    Because of the temporary existence of an extra spare P-4 larry
car, the new P-5 car is not utilized  to its maximum capability.
The significance of the larry  car availability, A, is weighted
by the amount of utilization as defined in Figure 55.

            U = _JL_ x 100                               (4)
                              202

-------
LARRY CAR PRODUCTION  INDEX
   The larry car production index relates the number of charges
made to the charging  times  used in calculating availability,
as indicated in Figure  56.
       --    T -  (B + M+ Mp + F + W2)
    This value should be  similar to the value given for
availability.  If  there was no extra spare larry car available,
the P.I. factor would be  expected to be greater than,  A, because
some repair time can be permitted without losing production.

MAINTENANCE AMP REPAIR REQUIREMENTS

    A daily record was maintained of all the maintenance and
repair  problems with the  required man hours by craft.   This work
has three classifications:
        1.  Breakdown repairs
        2.  Scheduled maintenance repairs
        3.  Design modifications (project work)

METHOD  OF OBTAINING DATA

    The battery turn foreman maintains a performance record for
each turn on a special form shown in Figure 58.  A project engineer
reviews the record, clarifies data with the production personnel,
and tabulates it on the daily summary sheet shown in Figure 59.

ANALYSIS OF RELIABILITY DATA

    The determination of  larry car performance was calculated
from the daily performance  data form shown in Figure 59.  The
summary figures for  the month of January  are  shown.  A graphical
relation is shown  in Figure 60.  The larry car was available
for satisfactory production operation 86.0% of the time which
compares with the  minimum criteria of 90%.  A summary of the type
of failures and the required man hours to perform the associated
breakdown repairs  or scheduled maintenance is shown on a monthly
basis in Tables 17, 18 and  18a.  The data for January  is further
detailed in
                   Table 19    Larry Car Failures
                   Table 20    Larry Car Maintenance
                              203

-------
ANALYSIS OF RELIABILITY DATA  (continued)

        Table 21    Operating Problems Preventing  Use  of
                    Larry Car

    This data does not account directly for problems with
charging wet coal which lengthens the charging time and makes it
more difficult to maintain the production schedule.

    Since the trend in car availability is still improving, it is
believed that an upper limit is about 90%.  After  the  addition
of jumper pipes, and an improved coal feed system, it  is believed
that this figure will be close to 95%.
                             204

-------
        Definition of Larry Car Production Index Factor
           P.I. =
                  T - (B + MI + Mp + F
where
P.I. =
           P =
           T =

           B =
          Ml =
          Mp =
           F =
larry car production index factor, per cent.
This represents the ratio of production charges
made with respect to the number of charges that
could have been made when the larry car was
available for charging.
number of production charges.
total number of scheduled charges  (full production
potential).
charges not made with this larry car because of
operating problems not associated with this
charging system reliability.  The nature of
these problems are discussed later in this section,
charges not made during time, m]_, that the car
was out of service for scheduled maintenance up
to the maximum limit of 8 hours/week.  Refer to
previous definition of "mj_".

charges not made during time, m    Refer to
previous definition of "nv,".
        charges not made during time, f.
        definition of "f".

        charges not made during time v>2 •
        previous definition of "v/2".
                                  Refer to previous
                                                  Refer to
                           Figure 56

                              205

-------
                                     OKL P-4
K5
O
61
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                               73  Ov°&*£!&
P-3 COAL,
                      OF
                                         ^o
                                                           &3-2S
                                          O
                                                             r>
                                                          Of
                                     37

-------
    j^.f.S.f
        Than
           CftA&GJBB
            fr/ffi
            CAR
                              ff
                                   MOT ?
                                      TIME .
                                     OUT OF
                                      REPAIR
                                      TIMS
             REPAIR
             MAJtffOUK
                                                                            REQUIRED
              3^8
             38
    2-2
t.
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52
t:?0
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tffR.
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SSMM
              38
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                             Offsr Of
                                                                         HOS-&
    23
     38
        V
               38
                                                  SB

-------
                     DAfL,y
                                                                                               JA.MUARY
 TURN
TOTAL,
        ff&s.
        Gff£Z
        CffO.
        743
ffKSMoT\ffR5MoT HRsNoT\HRS.Mo'i>tff&s.lIar\fXORMAL PKfOKfTy
 A/C
204.3
        CMG.
                CHS.
               XTR
              ScftED.
            iv. EXTRA
          !G
              PROJECT
              M.OVTFIC.
        18,25
      AFTEK,
      REPAIR;
                                         *£&L
70.5
I3.O
        HRS.
       lAZAir
        FOR,
                                                        RBPAtR
                                    HKS.
                                   WAfT
                                                 ftJSPAiKei

                                                  'fa)
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                             Hits.
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28.75
              ff&s.
              PK.O'D-
               CHG.
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              CHcf.
                                                               H&s.
                                  IOO
                                                                                     •sfc-
                                                                                          -2r X 100
                                                                                  -\ %#S.=
                                                                                                           -x/OO
                                                                                                   PRODUCTS out
               Cffc;.
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       i (?)
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 Oi)
 CHG.
MfSSED
ALL01V. PKOjeCT
MAtfJT. WORK
                            ivr/sse-p
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                     3. yjj\TT, PLACE CA& &Se&tfsi-&?fflay?
                                                                                3/3.7
                                                                   3r*/oo_-  3/3.7 =
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        .ScftJSD.
                 .
        . PROJECT
                            Kfffour)
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                                                           To &
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                                                            ,14.75

                                                            J_.0
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                                                             Q4.0
                                                            4-4-. 5
                                                        FIGURE 59

-------
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-------
Table 17.  TYPE OF LARRY CAR FAILURES AND REPAIRS

                   DECEMBER  1973
Item Type of Failure & Repair
1 Hydraulic leaks and hoses3
1_
2 Hydraulic actuators
3 Miscellaneous hydraulic
4 Damaged mechanical equip.
5 Environmental control unit
6 Defective or grounded wiring
7 Failure, repair, adjust
sensor
8 Hopper vibrator
9 Electrical problems in
control room
10 Miscellaneous electrical
11 Butterfly jammed0
Total
Repair
Man.Hr.
25.0
—
4.0
--
--
17.65
6.25
--
—
15.5
0.25
68.65
Ma int.
Man.Hr.
36.8
—
18.0
32.0
24.0
6.8
18.0
—
—
6.0
__
141.6
• •••••' •^^•••i n ,g „•„
Total
• Man.Hr.
61.8
0.0
22.0
32.0
24.0
24.45
24.25
0.0
0.0
21.5
0.25
210.25
  a.
  b
  c.
Does not include leaking or broken  hydraulic  actuators,
Leaking or mechanically damaged.
Operator normally frees the butterfly.
                            209

-------
  Table 18.  TYPE OF LARRY CAR FAILURES AND REPAIRS

                 JANUARY  1974
Item Type of Failure and Repair
1 Hydraulic leaks and hoses3
2 Hydraulic actuators
3 Miscellaneous hydraulic
4 Damaged mechanical equip.
5 Environmental control unit
6 Defective or grounded wiring
7 Failure, repair , ad just sensor
8 Hopper vibrator
9 Electrical problems in
control room
10 Miscellaneous electrical
11 Butterfly jammedc
Total
Repair
Man. Hr.
8.0
31.5
4.0
5.0
—
1.5
2.0
11.25
--
0.25
0.75
64.25
Ma int.
Man.Hr.
11.5
14.0
—
23.0
15.5
26.0
5.5
—
--
13.0
_ _
108.5
Total
Man.Hr.
19.5
45.5
4.0
28.0
15,5
27.5
7.5
11.25
0.0
13.25
0.75
172.75
a.  Does not include leaking or broken hydraulic actuators
b.  Leaking or mechanically damaged.
c.  Operator normally frees the butterfly.
                       210

-------
   Table 18a.  TYPE OF LARRY CAR FAILURES AND REPAIRS




                    February  1973
Item -Type -of Failure & Repair -
1 Hydraulic leaks and hoses3
2 Hydraulic actuators13
3 Miscellaneous hydraulic
4 Damaged mech. equipment
5 Environment control unit
6 Defective or grounded wiring
7 Failure, repair , ad just sensor
8 Hopper Vibrator
9 Electrical problems in
control room
10 Miscellaneous electric
11 Butterfly jammed0
Total
Repair
Man-Hr,
2.0
17.0
4.0
8.0
—
5.50
5.25
1.50
4.50
11.25
0.50
59.5
Ma int.
Man-Hr.
—
2.0
15.0
2.0
3.0
7.0
—
—
—
3.0
—
32.0
Total
Man-Hr.
2.0
19.0
19.0
10.0
3.0
12.5
5.25
1.5
4.5
14.25
0.5
91.5
a.  Does not include leaking or broken hydraulic actuators




b.  Leaking or mechanically damaged




c.  Operator normally frees the butterfly
                          210a

-------
Table 19.  LARRY CAR FAILURES
        JANUARY 1974
Item
1

2




3
4

5

6


7


8

9



10
11

12

13


14




Date
2

2




4
6

11

11


14


15

17

17

18
19

19

21


23




Turn
12-8

4-12




12-8
4-12

12-8

4-12


8-4


8-4

12-8

8-4

8-4
8-4

4-12

8-4


8-4




Description of Failure
#1 Butterfly jammed with coal
manually freed
460 VAC breaker opened,
adjusted pressure switch (#2
lid lifter dn) adjusted
limit arm (#1 lid lifter
extend)
460 VAC breaker opened
Adjusted pressure switch
#2 lid lifter down
#3 butterfly jammed,
manually freed
Pin sheared on #3 butterfly
actuator, looking for
trouble
Removed #2 butterfly
actuator , took to shop to
make new pin
Replaced Pin in #2 lid
lifter extend cylinder
Fuses blew twice in #1
vibrator- ran car without
Looked for trouble with
vibrator
Replace #1 vibrator
Removed broken pipe and
rethreaded
Replcaed 20 gal. of
hydarulic fluid
Anchor block came loose
causing #2 actuator to
move and break pipe
Replace broken hose, #2
hopper, replaced leaky hoses
#3 butter fly, replaced #2
actuator with spare (mount-
ing bolts sheared)
Repair
Craft
Oper.

Elec.




Elec.
Oper.

Repair
Man.Hr.
0.25

0.50




0.25
0.25

Oper. I 0.50

Mech.


Mach.


Mech.

1.0


14.0


2.0
|
Elec. 0.25
}
Elec. j 3.0

Elec.
Mech.

Mech.

Mech.


Mech.




8.0
1.5

4

7.5


12



1
          211

-------
Table 19.  LARRY CAR FAILURES
        JANUARY 1974
         (Continued)
Item
15



16

17

18


19

20
21

Date
25



27

27

28


28

30
30

Turn
4-12



12-8

8-4

8-4


8-4

8-4
8-4

Description of Failure
Lubricated and adjusted #1
lid lifter limit side arm
adjusted pressure switch
#2 lid lifter
Repaired ground to #2 lid
lifter magnet
Replaced leaky hose #2
butterfly
Replaced fuse #3 hopper,
straightened #1 hopper
level probe
Replaced leaking hose #3
butterfly
Replaced #1 retract limit
Removed damper arm, straight-
ened, and replaced
Repair
Craft
Elec.



Elec.

Mech.

Elec.


Mech.

Elec.
Mech.

i •
Repair
Man.Hr.
0.5



1.0

2.0

0.25


0.50

1.0
5.0

           211a

-------
Table 20.  LARRY CAR MAINTENANCE
          JANUARY 1974
—— — «•
Item
1



2


3



4



5



6



7





8


9




Date
3



3


4



4



8



8



9





9


11




Turn
8-4



8-4


8-4



8-4

4-12

8-4



8-4



8-4





8-4


8-4




Description of Scheduled
Ma int ena nee
Oscillating arms straightened
#1 lid lifter
Replaced two hydraulic hoses
(#2 butterfly, #3 lid lifter)
Replaced 3 worn shoes on
trolley poles, exercised and
lubricated remaining shoes
Removed, cleaned louvers on
environmental unit, renewed
flexible hose on exhaust
blower (louvers)
Found ground in 440 volt
junction box of car. also
partial ground in safety
switch at coal bin
Tried to remove pin from
leaking #2 lid lifter
extend cylinder - had to
re-assemble; could not free
Repair sticking limit on #3
lid lifter (contact lid) and
replaced bent side arm limit
on #2 lid lifter retract
Replace #2 lid lifter extend
piston and #1 lid lifter
raise piston (leaky) ; removed
and blew out clogged charcoal
filters in environmental
control unit
Replaced junction box covers
#2 lid lifter, adjusted #1
butterfly clockwise limit
Tighten loose nipple on #2
butterfly; Replace leaky tub-
ing with pipe nipples (#1 & 2
lid lifters) , welded nipples
to lid lifter frame
••••••••••••^••IHPBMi
Work
Craft .
Mech.



Elec.


Mech.



Elec.

Elec.

Mech.



Elec.



Mech .





Elect.


Mech.




V«VHHlWMIIiVMMI^H
Work
Man.Hr.
16



8


15.5



16

4

7



3.5



14





7


11.5




               212

-------
Table 20.  LARRY CAR MAINTENANCE
          JANUARY 1974
           (Continued)
Item
10
Date
11
Turn
8-4
Description of Scheduled
Maintenance
Replaced old wire to #1
vibrator with Micamat wire
Work
Craft
Elec.
Work
Man.Hr.
6
             212a

-------
Table 21.   OPERATING PROBLEMS PREVENTING USE OF LARRY CAR




                      JANUARY 1974
Item
1
2
3
4
5
Type of Operating Problem
No coal at south end of coal bin
Foreman elected to use spare car
#3 larry car being repaired at coal bin
No trained operator
Clean standpipes
Hours Spare
Car Used
53.45
46.85
11.0
31.6
61.4
204.3
                         212b

-------
                           APPENDIX   C

                   LEVELER BAR  INVESTIGATION

REPORT BY L. S. POPE, J&L RESEARCH

    Two coke oven leveler bars  failed in  service  at  Pittsburgh
Works P-4 Coke Oven Battery during the  installation  program of
the AISI coal charging system.  These two bars  were  of  new and
different designs (open web and solid web)  developed by Koppers
Company.  Both bars had been in service less than a  month before
failure occurred.

    Failure occurred when the bars became distorted  in  the
vertical direction such that they could no  longer fit through
the chuck doors in the coke ovens.  The open web  bar (design
number PF3724 Revision 5) displayed a rise  of about  6 1/4 inches
in the first 20 feet of bar starting at the nose  while  the solid
web bar (design number PF3724 Revision 11)  displayed a  rise of
about 8 1/8 inches in the first 23 feet back of its  nose*  (see
Figure 48 ).  Furthermore, the open web bar  has  buckled  in the
upper section about 10 feet from the nose (see  Figure 46 ).  No
cracks or mechanical defects were observed  in either bar.

    During normal operations these bars were used to level the
coal being charged into a coke oven.  They  normally  extended
about forty feet into the oven and oscillated on  about  a 20 feet
throw.  During such operation, the bars were either  unsupported
for the entire length extended into the oven or supported by
coal at points 8 feet, 21 ft. or 35 ft. from the  oven door by
the coal it was leveling.  These particular locations were the
positions of the chuck holes through which  coal was  charged and
under which conical piles of coal developed.  It  was these
piles that the bars leveled.
     These measurements were supplied by Karl Kortlandt of
     Development Engineering.

                            213

-------
   When bar failure occurred,  the solid web bar had suffered an
unusually long exposure**  in the interior of an oven.  The normal
exposure time is  2  to  3  minutes, but because of difficulties in
charging, the bar was  in the oven about eight minutes.  At the
next oven to be leveled  the  bar just barely cleared the roof upon
entering; normally, the  clearance is about 3".  This leveling
operation was normal with  a  3 minute exposure and the bar was
retracted with no difficulty.  At the next oven, however, the
bar could not be  inserted  because it had acquired an upward set
as described previously.

   With regard the open web bar there was no available failure
history other than  it  had  failed after less than a month in
service, and in significantly less time than the solid web bar.

MICROEXAMINATI ON

   Specimens for metallographic examination were obtained from
various locations in each  bar.  The examination revealed that
the microstructure  in  all  areas was about the same and typical
of as  hot rolled  plain carbon structural steel, i.e. equiaxed
ferrite grain size  of  ASTM #8 with about 15% pearlite  (see Figure
61) .   No evidence was  uncovered to  indicate that  the bars were
overheated  (heated  above 1350°F) in the oven.  The inclusion
morphology  in each  case  indicated the rolling direction of the
original sections was  along  the length of the bars.

CHEMICAL ANALYSIS

   Chemical analyses  were also performed on both bars and the
results are presented  in Table 22. The analyses for all sections
were  similar and  conformed to the specifications of ASTM A-36
structural  steel.   The absence of significant amounts of aluminum
indicated that this steel  was probably silicon semi-killed.
  **
Such exposure times only occurred  infrequently  when charg-
ing the first eight ovens of the battery which,  because of
construction, were charged with an inferior  spare larry car,
                             214

-------
MECHANICAL TESTING

    Tensile tests were performed on  specimens obtained from  the
web of the open web bar in the region where  buckling occurred
 (top and bottom sections).*  Both  tests  conformed  to the  tensile
specifications of ASTM A-36 structural steel  although there were
slight differences in the strength properties of the two  areas
 (Table 23).

DISCUSSION

    There were no metallurgical defects  or  irregularities  in the
steel of either bar.  Both materials were typical  of hot  rolled
plain carbon steel and met all the specifications  of ASTM A-36
structural steel.  Microexamination  revealed  no  evidence  to
indicate that the bars had been subjected to  any unusual  thermal
cycles involving temperatures above  1350°F.   However,  because
this type of microstructure is not reflective of low temperature
thermal treatment we could not speculate as to any thermal cycle
experienced below 1350°F.

    The failure of these bars is believed to  be  due to a
thermal expansion effect resulting from  non-uniform heating
of the bars while they were at least partially supported  by
coal in the oven.  For both bars,  four actual thermal -
mechanical situations were possible  as indicated below.

    (1) If the bars had been supported by coal and heated
        uniformly, expansion or lengthening of the bars would
        have been uniform and no distortion would  have occurred.

    (2)  If the bars had not been  supported by coal and still
         heated uniformly,  thermal growth would  have been  uniform.
         Furthermore, analysis indicates that if the temperature
         exceeded 1100°F, the bars could not  support their own
         weight.  But, such a distortion would have been  downward,
         opposite to that actually observed.

 * Tensile tests were not performed  on the  solid web bar  since
   removing the material necessary for such tests  would have
   destroyed the structural integrity of the  bar.   Such destruc-
   tion was not considered advisable at  the time.

                             215

-------
DISCUSSION (continued)

    (3)  If the bars had not been supported by coal and heated
        non-uniformly the  tops  of the bars would have been at
        a higher temperature  than the bottoms since the tops
        would have seen radiant heat from the oven roof while
        the bottoms would  not have seen any radiant heat from
        the freshly charged coal.   Such a situation would have
        resulted in a downward  deflection.  Furthermore, this
        deflection would have recovered upon cooling.

    (4)  If the bars had been  supported by coal and heated
        non-uniformly it is believed that the failures actually
        observed would have occurred as described below.

    The failure mechanism proposed is the fourth case where the
bars suffered differential  thermal expansion which resulted in
vertical distortion.  In the region of failure (last 20 to 25 ft.
of both bars) the top of each  bar is believed to have been
significantly hotter than the  bottom.   The bottom was at least
partially resting on coal in the oven so that downward deflection
was restrained.  With this  restraint,  the bars were unable to absorb
the differential thermal elongation from top to bottom by a down-
ward deflection.  Some of the  differential length was absorbed
by elastic compression at the  top and  elastic tension at the bottom.
With the top of the bar hotter than the bottom,  the top also
possessed a lower yield strength.   Therefore, when additional
strain had to be absorbed the  top suffered plastic (permanent)
compression while the bottom suffered  additional elastic
(recoverable) tension.  The open web bar was unable to support
the 00repressive load and it therefore buckled; whereas the solid
web bar suffered plastic compressive strain.  When the bar was
removed from the oven and cooled down so that the top in each
case was at the same temperature as the bottom the top became
shorter than the bottom due to either  the buckling or plastic
compression suffered at the higher  temperature.   The bars absorbed
this differential length by deflecting upward and thereby putting
the shorter top on a shorter arc than the bottom.  When the bars
cooled upon removal from the ovens,  the upward deflection was not
significantly restrained.
                              216

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DISCUSSION  (continued)

    Sample calculations for this proposed  mechanism for the
solid web bar, assuming the top reached  a  temperature between
1000°F and 1250°F, showed that the  temperature  differential
would have had to be between 460°F  and 320°F.

    Without a detailed thermal analysis  or actual  temperature
measurements, it can not be clearly established that such  temper-
ature differentials can in fact occur.  However,  the failure
history and design considerations support  this  hypothesis.

    The solid web bar obtained its  upward  distortion gradually
and at least partially outside any  oven.   It obtained some dis-
tortion after the eight minute exposure  and before leveling the
next oven.  Between this next oven  and the oven it could not
enter it obtained additional distortion.   This  comports well with
the concept of a bar cooling and distorting upward,  as  it cools.

    A comparison was made between the design of this solid web
bar and the design of a bar which had given satisfactory service
for more than fifteen years prior to being replaced by  this solid
web bar (see Figure 62).  Thermal consideration of both designs
indicated a probable reason why the solid  web bar  failed while
the old design bar had not failed even though it saw similar
service including long time exposures in the interior of the ovens.
The solid web bar had considerably  more  top surface area exposed
to radiant heat than the old design.  In addition  the solid
web bar also had considerably less  mass  along its  vertical length
to carry away heat from the top surface.   Furthermore,  the
situation with the open web bar was even more extreme since it
had the same area exposed to roof radiation as  the solid web bar
but almost no web to carry heat from the top surface.   This fact
may explain why the open web bar failed  more rapidly than the
closed web bar.

    The thermal differentials proposed could have  resulted from
the exposure of the top of the bars to greater  radiant  heat than
the bottom.  The tops of the bars would  see radiant heat from
the roof which the bottoms would not.  In  fact,  the bottoms of
the bars could have been buried in  coal  and insulated from any
radiant heat.  The design considerations discussed above indicate
why such a thermal imbalance would  not be  corrected by  internal

                               217

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DISCUSSION (continued)

conduction through the webs of the bars.

CONCLUSIONS

    (1) There ware no material defects  in  either  bar.   The
       steel in both bars met the specifications of ASTM A-36
       structural steel.

    (2) No evidence was present to indicate  that  the failures
       were caused by overheating.

    (3) Failure was caused by differential heating in  the bars
       resulting from an interaction between  the design  of  the
       bars and long exposure times in the  coke  ovens.

    To prevent similar failure in the future,  several  recommenda-
tions should be followed.

    (1) Set a maximum exposure time in  each  oven  to eliminate
       excessive heating of the bars.   This should become more
       practical after the use of the  inferior larry  car is
       discontinued and the incidence  of  charging hole plug-up
       is eliminated.

    (2) Redesign the bars to eliminate  excessive  heat  buildup
       in the top surface or employ the old design bar which
       calculations now show is usable with the  AISI  improved
       procedure1.
  1
   K. R. Kortlandt, "AISI Coal Charging  System,  Coke Oven
   Leveler Bar," memo to J. H. Stoltz dated  December 9,  1971.

                              218

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Table 22.  CHEMICAL ANALYSIS
ASTM A-36 specification
Solid web leveling bar
Test from 1' location
Test from 41' location
Open web leveling bar
(WEIGHT %)
C
.26
max
.21
.20
.21
Mn
—
.74
.74
.64
Si
--
.033
.035
.033
S
.05
max
.022
.024
.017
P
.04
max
.006
.006
.012
Al
--
.005
.005
.005
O
--
—
--
.091

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Table 23.  MECHANICAL TEST RESULTS

ASTM A-36 specification
Open web leveling bar
Unbuckled web
Buckled web
Yield
Strength
(.2% offset,psi)
36,000
min
44,400
40,400
Tensile
Strength
(psi)
58,000/
80,000
72,840
64,530
Total
Elongation
(% in 2")
23 min.
38.0
35.5
Uniform
Elongation
(°/o)
-
26.5
26.5

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             MICROSTRUCTURE - LEVELER BAR STEEL

MICROSTRUCTURE TYPICAL OF THE STEEL IN BOTH NEW BARS - TYPICAL OF
AS HOT ROLLED PLAIN CARBON STEEL.

ETCHANT: 2%NITAL 200X
                          FIGURE 61
                              221

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THE

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REPORT BY N. C. DeLUCA, J&L RESEARCH

INTRODUCTION

    In conjunction with the AISI/EPA coal charging  system  at the
Pittsburgh Works By-Product Department, Koppers  installed  a new
light-type leveler bar.  Koppers believed that the  light-type
leveler bar was necessary to enhance the ability of the bar to
support itself in the coke oven whenever the normal coal charge
upon which the bar rests was absent.  Subsequently,  two of the new
light-type leveler bars failed by assuming an upward deflection of
8 inches along the first 20 feet of the length of the bar.  Since
the failures appeared to be the result of overheating and/or
uneven heating of the bars, a study to characterize the thermal
cycling of the bars was conducted. 1

PRELIMINARY STUDY

    In the preliminary study a contact pyrometer was used  to measure
surface temperatures along the length of the old heavy-type leveler
bar.  The old heavy-type leveler bar was chosen  for this
study because both of the light-type leveler bars supplied by
Koppers were warped and out of service.  In addition, the
continued use of the old heavy-type leveler bar was under
consideration as it had performed well in service since the
construction of P-4 battery.

    The surface temperatures were measured after normal and
extended coke oven leveling operations.  The purpose of these
measurements was to locate the critical areas or hot spots of
the bar2.

    Typical temperature distributions along the  length of  the bar
are shown in Figure 63.  in addition, a typical  temperature

 1
   Memo, L.S.  Pope  to  J.H.  Stoltz,  "Coke  Oven  Leveler  Bar,
   Service Job No.  61-71",  1/19/72.

 2 Memo, N.C.  DeLuca to E.A. Mizikar,  "Status  of the Coke  Oven
   Leveler Bar Program", 4/20/72.

                             223

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PRELIMINARY STUDY  (continued)

distribution along both the length and width  of  the  bar  is  shown
in Figure 64.  The temperature peaks located  along the bar  are
related to the position of the coke oven  charging holes  over the
leveling bar when the bar is fully extended into the oven.  As
shown in Figure65 the highest temperature occurred directly
under the No. 3 charging hole and the second  highest temperature
was under No. 2 charging hole.
FINAL STUDY

    In the final study with the heavy-type  leveler bar, continuous
temperature measurements were taken at the  location  shown  in Figure
66.  The measuring sites were selected on the basis  of  the surface
temperature measurements obtained in the preliminary  study.  The
function of each measuring site was as follows:

Site 1 - To measure the nose temperature of the bar  and to
         determine the^T between the nose and the hottest
         location of the bar.

Sites 2, 3 and 4 - To measure the temperature at the hottest
         location of the bar and to determine the AT between the
         top and the bottom of the bar.
Site 5 -
Site 6 -
To determine the AT between the hottest location and a
point on the bar that is the same distance from the hot
spot as No. 1 but toward the rear of the bar.

To measure the temperature of the secondary hot spot of
the bar.
Site 7 - To measure the temperature of the bar between  the No. 1
         charging hole and the ascension pipe.

NOTE:  The thermocouple at Site No. 4 failed  shortly after installa-
       tion

    The leveler bar temperature measurements  were obtained by
inserting 1/16", sheathed, type K thermocouples  into holes drilled
in the leveler bar, as illustrated in Figure  66.  The holes were
first drilled through the leveler bar, then the  opening on the

                              225

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FINAL STUDY  (continued)

surface to be measured was tack welded  shut  to  insure that  the
thermocouple measuring junction would be  in  close  contact with the
surface after its insertion.  The seven thermocouples embedded
in the leveler bar were fed back along  the top  of  the bar through
a 1/2" protection tube to a thermocouple  switching unit.  The
switching unit, illustrated in Figure 67, multiplexed the seven
thermocouple outputs into a single pulsed output.   The output,
a series of 3-second pluses interrupted by a sequencing pulse, was
carried over thermocouple extension wire  to  a continuous strip
chart recorder.  A weight driven thermocouple wire retracting
reel, also shown in Figure 67, permitted  a 40 ft.  movement  of
the leveling bar while the temperatures were being recorded.

    During the final study, 106 coke oven leveling operations and
the cooling periods between the operations were recorded.   The
leveling operations that were monitored included normal and
extended operations, up to 16 minutes,  utilizing both the No. 3
table-fed and the No. 4 gravity-fed larry cars  and both the high
and the low steam pressure adapted coke ovens.

RESULTS AND CONCLUSIONS

    The information gathered in monitoring the  leveling operations
was partially analyzed by both multiple regression and graphical
methods before the analysis of the data was  curtailed by a  change
in project priorities.  The multiple regression model and the
data will be kept on file at Graham Laboratory  for future analysis
if required.

    The data gathered from 106 leveling operations consists of
approximately 5,000 time-temperature data points for  the heating
cycles and 18,000 time-temperature data points  for the cooling
cycles.  In addition to the time-temperature relationship,  the
following information was also obtained for  each operating  cycle:
the heating time, the larry car, the steam pressure,  the number
of strokes, the oven number, and the cooling time  until the next
operation.  The data were first subdivided into heat-up and cool-
down segments.  Multiple regression analyses and individual cycle
graphing were then performed for both the heat-up  and the cool-
down data.
                              229

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-------
MULTIPLE REGRESSION ANALYSIS OF THE HEAT-UP  DATA

    A summary of the leveler bar heat-up  data  given in Table  24
was generated by multiple regression analysis  of the raw data.
The table illustrates that the heat-up  time  of a single leveling
operation ranged from 0.88 minutes to 16.9 minutes  with an  average
leveling time of 2.92 minutes.  The table also illustrates  that
the temperature of the leveling bar ranged from 200°F to 1160°F.
Within these confines, the initial bar  temperatures ranged  from
an average of 354°F at site 1 to an average  of 485°F at site  7
and the final temperatures ranged from  an average of 398°F  at site
1 to an average of 592°F at site 2.  These averages reflect the
anticipated temperatures during normal  leveling operations.

    The results of the multiple regression analysis for the final
leveling bar temperatures are listed in Table  25; the details
of the analysis are described on page 244.     As Table 25
illustrates, the initial temperature at the  site is the largest
single factor in accounting for the final temperature;  it represents
from 55 to 76% of the variability.  The next largest factor in
accounting for the final temperature is Cheating time,  which
together with the initial temperatures  represents from 83 to  87%
of the variability.  The final temperature at  site  1 differs  from
the other sites in that its final temperature  is not significantly
related to heating time,   but is almost completely  explained  by
initial temperature.  A likely explanation for this relationship
is that the bar is advanced along with  the smoke box to a position
directly in front of the chuck door to  await the start of the coal
charging.  In this position the nose of the  bar is  exposed  to direct
radiation from the coke oven while the  rest  of the  bar is still
outside the oven.  Thus,  the manner in  which the nose is heated
is significantly different from the rest of  the bar.   The other
variables that affect the final temperature  of the
bar are the larry car and the number of strokes during charging.
They respectively account for 4% and 2% of the variability  of the
final temperature.  Thus, with the exception of site 1 at the
nose of the bar, the four variables: initial temperature,
 yhea'ting" time",  larry car.  and number of strokes, together  account
for 88 to 91% of the variability in the final  temperatures.   No
other variable significantly enters into  the explanation of
final temperature under normal operating conditions.  Notably
absent was the steam pressure, as it was  feared that the high
steam pressure necessary with the new charging system would
unduly heat the leveling bar under normal operating conditions.


                             231

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Table 24.  PARTIAL SUMMARY OF LEVELER BAR HEAT-UP DATA
Variable
Heating time (min.)
Strokes
Steam pressure
l=low, 2=high
Larry car no.
Initial temp.°F 1
Initial temp.°F 2
Initial temp.°F 3
Initial temp.°F 5
Initial temp.°F 6
Initial temp.°F 7
Final temp.°F 1
Final temp.°F 2
Final temp.°F 3
Final temp.°F 5
Final temp.°F 6
Final temp.°F 7
Average
2.92
7.23
1.56
3.15
354
469
452
478
404
485
398
592
546
570
474
555
Sigma
2.16
4.97
0.49
, 0.35
80
152
145
141
111
147
88
166
158
147
117
164
Minimum
0.88
3.0
--
--
200
215
210
210
210
240
260
287
263
273
283
270
Maximum
16.9
30.0
—
—
580
950
960
990
745
945
635
1160
1070
1030
870
1080
                        232

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             Table 25.  RESULTS OF  THE REGRESSION ANALYSIS  FOR THE
                         FINAL LEVELING BAR TEMPERATURES

Standard deviation
of the raw data
1st variable in
model
% of variability
accounted for
2nd variable
in model
Comulative % of var-
iability accounted foi
3rd variable
in model
Comulative % of var-
iability accounted for
4th variable
in model
Cumulative % of var-
iability accounted foi
Final standard
deviation
Site #1
88°F
initial
temp.
76%
number
of stroks
88%
larry
car
89%
--
89%
28°F
Site #2
166°F
initial
temp.
55%
>/time
83%
larry
car
87%
number
of stroks
88%
59°F
Site #3
158°F
initial
temp.
59%
VETme
82%
larry
car
88%
number
of stroks
89%
53°F
Site #5
147°F
initial
temp.
64%
VtTme
87%
larry
car
91%
--
91%
43°F
Site #6
117°F
initial
temp.
60%
•«/tTme"
86%
larry
car
88%
number
of stroks
88%
40°F
Site #7
164°F
initial
temp.
64%
*/time
78%
larry
car
85%
number
of stroks
87%
60°F
OJ
00

-------
MULTIPLE REGRESSION ANALYSIS OF THE HEAT-UP DATA  (continued)

    Additional  multiple regression analyses were run using the
delta  temperatures and the rates of temperature rise as the depend-
ent variable.   Other than the initial temperatures being a signifi-
cant factor,  the results were mixed with the exception that the
strokes per minute was the second most significant factor affect-
ing the rate  of temperature rise.  An inverse relationship exists
which  dictates  that the more often the bar is stroked per minute
the slower the  rate at which the bar will heat.  This relation-
ship is best  explained by considering the ratio of time the
bar spends in the oven to the time the bar spends out of the oven
during a single stroking cycle.  If the ratio were 1:1 the rate at
which  the bar was stroked should have little significance; but
this is not the case in actual practice.  Usually the operator
extends the leveler bar, pauses, then retracts the bar.  The bar
is retracted  from 20 feet to full stroke and then immediately
re-inserted into the coke oven.  The pause in the oven is the
longest when  the bar is stroked the least number of times per
minute.  Thus,  by stroking the bar more frequently or by not paus-
ing in the oven the rate of temperature rise of the bar can be
reduced.

GRAPHICAL ANALYSIS OF THE HEAT-UP DATA

    The leveling bar 'temperature at site 2 was plotted as a func-
tion of the heating time for some of the leveling operations.
These  graphs  are illustrated in Figures 68, 69, 70 and 71 for
the No. 3 and No.4 larry cars charging under high and low pressure
steam.

    The graphs  in general illustrate some of the inconsistencies
in the leveler  bar heating during a coke oven charging.  These
inconsistencies are readily apparent in Figure 70, in which
under  similar operating conditions the temperature of the bar
increased in  different fashions, and in one case  (C) actually
decreased during the leveling operation.  The manner in which the
leveler bar heats is related to the manner in which the coal enters
the coke oven.   The coal being cooler than the levelling bar tends
to cool the bar when it is dropped quickly and when air is
restricted from entering the coke oven through the charging holes.
A comparison  of Figure 68 with Figure 69 and Figure 70 with
Figure 71 demonstrates that the No. 3 larry car is more efficient
                              234

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GRAPHICAL ANALYSIS OF THE HEAT-UP DATA  (continued)

in charging the coal and in limiting the temperature rise of the
leveler bar.  This observation agrees with the multiple regression
analysis, which found that next to the  initial temperature of
the bar and the heating time, the larry car was the most
important factor in the leveling operation.  Along with this
condition the No. 4 larry car usually takes longer to charge an
oven and thereby reinforces the conviction that the No. 4 larry
car should be used no more than absolutely necessary.

    The graphs also support the conclusion that the steam
pressure is of little consequence in the heating rate of the
leveler bar.  A comparison of Figure 68 with Figure 70 and
Figure 69 with Figure 71 shows no significant difference between
high and low steam operating conditions.

    Two abnormally long leveling operations are illustrated in
Figure 72.  Curve A represents a leveling operation using No. 4
larry car from which the coal would not feed properly; air was
entering the charging holes during the  entire operation.  The
temperature of the bar climbed steadily during the entire
leveling operation.  In contract Curve  B represents a leveling
operation using the No. 3 larry car in which the leveler bar was
deliberately permitted to remain in the  oven after the coal charg-
ing was complete.  In this case the covers were replaced on the
charging holes after the larry car was  emptied in order to
prevent the entrance of air into the oven.  The temperature of
the bar climbed steadily until the covers were replaced and then
began to drop slightly, possibly as a result of being in contact
with the cooler coal.  This comparison  illustrates the importance
of replacing the charging hole covers as quickly as possible in
the event that the leveler bar must remain in the oven due to an
equipment failure.

    The rate of temperature rise of the leveling bar fluctuates
during a normal leveling operation in response to the oven
conditions; the worst case heating of the bar is usually evident
only for short periods of time during the leveling operation.
Figure 73 contains a composite graph of the leveler bar temperature
which was constructed by combining the  worst case heating segments
from the graphs of numerous leveling operations.  The graph
illustrates that a leveler bar with an  initial temperature of

                              239

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GRAPHICAL ANALYSIS OF  THE  HEAT-UP DATA (continued)

450°F could reach a  1000°F temperature limit in 6.5 minutes if the
worst case observed  heating conditions exist for the duration
of the leveling operation.   While this situation is highly unlikely,
it is possible for the temperature to exceed 1000°F if the leveler
bar has a high initial temperature and is heated for a short
period under worst case conditions.

   The graph in Figure 74 gives the maximum initial temperature
of the leveler bar as  a function of the safe heating time under
the worst case heating conditions.  To reduce the possibility of
the leveler bar reaching 1000°F,  the normal operating time should
be within the safe heating time.   During the 106 operations that
were monitored, the  average leveling time was 2.92 or approximately
3 minutes.  As can be  seen in Figure 74,  a normal 3 minute level-
ing operation would  be safe under the worst case heating conditions
as long as the leveling bar was  initially below 800°F.

   This criterion would have prbhibited the leveling operation
(A) illustrated in Figure  72 which began with an initial temperature
of 875°F and reached a final unsafe leveler bar temperature of
1160°F.

RECOMMENDATIONS

   To substantially reduce the  risk of overheating the leveler
bar, 800°F should be adopted as  the maximum initial temperature
with which a leveling  operation  can be performed.  The 800°F
criterion can be utilized  by having the operator check the leveler
bar temperature with an 800°F Tempilstik whenever he suspects the
bar is in danger of  overheating.   He should definitely check the
bar after every extended leveling operation.  To check the bar
temperature, the operator  should rub the Tempilstik on the top of
the bar 5 feet back  from the nose; the location is directly
opposite the operator's door.

   Implementation of  this procedure along with limiting the
operating time of the  leveler bar to 3 minutes in cases where the
bar has recently been  heated to  above 800°F will substantially
reduce the risk of overheating the leveler bar.  To completely
eliminate all risk of  overheating would require a somewhat
impractical procedure  of establishing a time limit on the operation
based upon a difficult measurement of the bar's initial temperature.
                              242

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MULTIPLE REGRESSION ANALYSIS OF HEAT-UP DATA

    To  conduct  a multiple regression analysis the following infor-
mation  was  punched  on IBM cards using one card for each operating
cycle:

1   The coke  oven number
2   Dummy number  (part of the coke oven number)
3   The heating time of the cycle
4   The number  of leveling strokes during the cycle
5   The steam pressure (either high or low)
6   The larry car used (either #3 or #4)
7   The initial temperature at site #1
8   The initial temperature at site #2
9   The initial temperature at site #3
10  The initial temperature at site #5
11  The initial temperature at site #6
12  The initial temperature at site #7
13  The final temperature at site #1
14  The final temperature at site #2
15  The final temperature at site #3
16  The final temperature at site #5
17  The final temperature at site #6
18  The final temperature at site #7
19  The cooling time till the next cycle

    Using the punched data the following additional variables were
generated during the regression analysis to provide a larger
basis for correlation:

20  The temperature change (DELTA TEMP) at site #1
21  The temperature change (DELTA TEMP) at site #2
22  The temperature change (DELTA TEMP) at site #3
23  The temperature change (DELTA TEMP) at site #5
24  The temperature change (DELTA TEMP) at site #6
25  The temperature change (DELTA TEMP) at site #7
26  The average rate of temperature rise at site #1
27  The average rate of temperature rise at site #2
28  The average rate of temperature rise at site #3
28  The average rate of temperature rise at site #5
30  The average rate of temperature rise at site #6
31  The average rate of temperature rise at site #7

                               244

-------
MULTIPLE REGRESSION ANALYSIS OF HEAT-UP DATA  (continued)

32  The average strokes per minute during  the  cycle
33  The inverse time  (1/T)
34  The square root of the time  ( ^T)
35  The square of the time(T2)
36  The inverse square root of the time
37  The inverse square of the time
    The multiple regression analysis provides  three  outputs: a
summary listing of the variables containing  the  average,  sigma,
minimum and maximum values; a full correlation matrix  listing
of the correlation coefficients for the relationships  between
all the variables; and regression equations  giving a chosen
variable as a function of the other variables.

    The summary listing of all the measured  variables  is  illustrat-
ed in Table 26. The table lists the variables  by name  and number
and gives the average, the sigma, the minimum  and the  maximum
values.  The minimum and maximum values are  given in exponential
form.

    The full correlation matrix listing of the correlation coeffi-
cients for the relationships between all the variables is illustrat-
ed in Table 27.  The variables are listed by name and  number along
the side of the matrix and by number along the top of  the matrix.
The value listed at the intersection of the  horizontal and the
vertical lines representing two variables is the correlation
coefficient.  This coefficient can range from  .000 which  represents
a random relationship between the variables  to 1.000 which
represents a direct relationship between the variables.   A
correlation coefficient of .25 or greater is generally considered
significant and the variable should be included  in the potential
model .

    The potential model is a regression equation which explains
a chosen variable in terms of the other variables.   In the leveler
bar study the final temperature was chosen to  be the dependent
variable which was to be explained by the independent  variables:
heating time, strokes, strokes per minute, steam pressure, larry
car.- initial temperature of the bar, and the mutations of heating
time.  in choosing the independent variables,  interrelated


                             245

-------
MULTIPLE REGREASION ANALYSIS OF HEAT-UP DATA (continued)

variables must be  avoided;  for example, the final temperature
should not be determined as a function of the delta temperature
and the initial  temperature since the delta temperature was
calculated from  the final temperature and the initial temperature

    The potential  model for the final leveler bar temperatures
at the hottest location, measuring site 2 was:
Final        =(.725)  initial temp. + (214)  heating time +  (92.7)
temperature
              larry  car number - (4.90) number of strokes -357°F
                               246

-------
                                   TABLE 26
VARIABLE
                             AVERAGE
                                              SIGMA
                                                         MINIMUM
                                                                        MAXIMUM
I
2
1
4
b
6
7
n
9
10
1 1
12
13
14
lr.
16
17
11
19
20
21
2?
23
24
21!
26
27
2P
2 3 1 3
.9907?
. H96'I6
.37769
.15137
.21 729
.28320
.31177
.H'if)77
.54720
.4246?
.0944 I
.55667
. 33023
. 320HO
. 4 ? 89 I
.22470
^ p f\ 4 :j £
.68431
.07597
.0?.705
.59^52
.43848
.64299
.20122
.64648
.22702
0
e
p
4
0
0
80
152
145
141
111
147
88
166
158
147
117
164
n
42
114
102
90
75
99
12
28
26
22
20
28
0
0
0
33
C
C
.82094
.09241
.16560
.97527
.49797
.35969
. 79964
.22006
. 34319
.80518
.46675
. 89450
. 16003
.04910
.20053
.0671B
. 1 73CO
.40817
.43555
. 7973B
.91956
.PR657
.68958
.08730
.71542
.41218
.68787
.23654
.066 35
. 362C3
.B5469
.94371
.18732
.47720
.44226
. 144C1
.19930
1.
1.
8.
3.
1.
3.
2.
2.
2.
^ a
2.
2.
2.
2.
2.
2.
2.
2.
0.
-5.
-8.
-6.
-3.
-e.
-e.
-2.
-3.
-2.
-1.
-4.
-3.
I.
5.
9.
7.
2.
3.
OOOOOE
OOOOOE
00
00
80COOF-01
OOOOOE
COOOOF
OCOCOE
CCOOOF.
15000E
IOOCOE
lOOOOt
IOOOOE
40COOF.
60000E
07COOE
63000F
73000E
82000E
70000E
0
OCOOOE
COCOOE
OOOOOE
5CCCOF.
COOOOE
500COC
17391E
96040E
97030E
4462HE
4943BE
69565E
09091E
00
oo
00
02
02
02
0?
02
0?
02
02
02
02
02
02

01
01
01
01
01
01
01
01
01
01
01
01
00
H9623E-02
38083E-01
74400E-01
42H22E-01
47655E-03
3.
2.
1.
3.
2.
4.
5.
9.
9.
9.
7.
9.
6.
I.
1.
1.
8.
1.
5.
2.
4.
4.
4.
3.
4.
6.
1.
9.
9.
7.
1.
5.
1.
4.
2.
1.
1.
OOOOOE
70000E
69600E
OOOOOE
OOCOOE
OOOOOE
noooofi
50000E
60000E
9COOOE
45000E
45000E
35000E
I6000E
07000E
03000E
7UOOOE
OHOOOE
50200E
30000E
90000F
2bOOOE
50COOE
35000E
35000E
41026E
29825E
69R28E
Obi 72E
32759E
03448E
68182E
13636E
11825E
87641E
06600E
29132E
00
01
01
01
CO
00
02
02
02
02
02
02
02
03
03
03
02
03
01
02
02
02
0?
02
02
01
0?
01
01
01
02
00
00
00
02
CO
00
                                Leveler Bar Study
               Summary of Leveler Bar Heat-up Data - 106 Observations
                                      247

-------
1

3
4
5
6
7,
R
9
10
11
12
13
14
15
16
17
18
19
20
21
22
23
24
25
26
27
28
29
30
31
32
33
34
35
36
37
8
9
10
11
12
13
14
15
16
17
ta
19
20
21
22
23
24
25
26
27
28
29
30
31
32
33
34
35
36
37
OVEN NO.
DUMMY NO
HEATING TIME
STROKES
STEAM PRESSURE
LARRY CAR
INITIAL TEMP I
INITIAL TEMP 2
INITIAL TEMP 3
INITIAL TEMP 5
INITIAL TEMP 6
INITIAL TEPP 7
FINAL TEMP 1
FINAL TEMP 2
FINAL TEMP 3
FINAL TEMP 5
FINAL TEMP 6
FINAL TEMP 7
COOL TIME
DELTA TEMP 1
DELTA TEMP 2
DELTA TEMP 3
DELTA TEMP 5
DELTA TEMP 6
DELTA TEMP 7
RATE TEMP. RISE I
RATE TEMP. RISE 2
RATE TEMP. RISE 3
RATE TEMP. RISE 5
RATE TEMP. RISE 6
RATE TEMP. RISE 7
STRCKES/MIN
INVERSE TIME
RCOT TIME
SQR TIME
INVERSE ROOT TIME
INVERSE SQR TIME
INITIAL TEMP 2
INITIAL TEMP 3
INITIAL TEMP 5
INITIAL TEMP 6
INITIAL TEVP 7
FINAL TEMP 1
FINAL TEMP 2
FINAL TEMP 3
FINAL TEMP 5
FINAL TEMP 6
FINAL TEMP 7
COCL TIME
DELTA TEMP 1
DELTA TEMP 2
DELTA TEMP 3
DELTA TEMP 5
DELTA TEMP 6
DELTA TEMP 7
RATE TEMP. RISE 1
RATE TEMP. RISE 2
RATE TEMP. RISE 3
RATE TEMP. RISE 5
RATE TEMP. RISE 6
RATE TEMP. RISE 7
STRCKES/MIN
INVERSE TIME
ROOT TIME
SQR TIME
INVERSE RCCT TIME
INVERSE SQR TIME
TABLE 27
I
1.000
•0.051
•0.148
0.112
0.773
0.250
0.011
0.008
0.029
•0.034
•0.020
•0.040
0.015
0.052
0.037
0.049
•0.060
•0.008
0.101
0.050
•0.064
0.015
0.027
•0.063
0.047
0.229
0.045
0.112
0.137
0.083
0.154
0.054
0.025
•0.120
•0.166
0.050
0.003
8
I. 000
0.994
0.964
0.866
0.931
0.422
0.743
0.758
0.796
0.705
0.665
0.130
0.192
0.252
0.240
0.216
0.184
0.284
0.392
0.498
0.467
0.459
0.396
0.457
0.303
0.099
0.115
0.117
0.103
0.095
2

1.000
-0.236
-0.147
-0.267
0.263
-0.323
-0.073
-0.038
-0.077
-0.215
0.013
-0.322
-0.025
-0.000
-0.039
-0.235
0.071
0.018
-0.053
0.061
0.053
0.058
-0.047
0.097
0.130
0.299
0.254
0.307
0.145
0.243
0.152
0. 155
-0.227
-0.219
0.180
0.118
9

l.OOC
0.956
0.852
0.949
0.401
0.751
0.773
0.799
0.696
0.693
-0.134
-0.183
-0.231
-0.223
-0.199
-0.177
-0.266
-0.384
-0.470
-0.446
-0.434
-0.386
-0.437
-0.322
-0.095
0.115
0. 120
-0.099
-0.092
3


l.OCO
0.846
0.152
0.179
0. 137
0.121
0.121
0.104
0.099
0.143
0.420
0.584
0.538
0.535
0.562
0.461
-0.092
0.606
0.683
0.655
0.7C6
0.723
0.548
-0.022
0.077
0.118
0.1CO
0.109
0.126
-0.174
-0.703
0.974
0.937
-0.8C3
-0.528
10


l.COO
0.937
0.848
0.557
0.680
0.688
0.803
0.755
0.556
-0.121
-0.167
-0.295
-0.293
-0.261
-0.210
-0.340
-0.360
-0.545
-0.527
-0.514
-0.433
-0.517
-0.170
-0.089
0.101
0.097
-0.092
-0.086
4



1.000
0.084
0. 150 '
0.255
-0.018
-0.029
0.042
0.068
-0.059
0.555
0.392
0.335
0.442
0.520
0.206
-0.039
0.663
0.591
0.. 556
0.651
0.704
0.428
0.142
0.071
0.102
0.152
0.191
0.074
0.294
-0.626
0.845
0.750
-0.715
-0.460
11



1.000
0.696
0.682
0.576
0.569
0.724
0.781
0.410
-0.1CO
-0.165
-0.314
-0.328
-0.292
-0.263
-0.356
-0.360
-0.567
-0.565
-0.547
-0.520
-0.525
-0.130
-0.112
0.105
0.081
-0.111
-0.110
5




1.000
- -0.269
0.050
-0.019
-0.012
-0.007
0.030
-0.014
0.039
0.045
0.033
0.027
0.104
-0.008
-0.092
-0.014
0.090
0.068
0.056
0.117
0.008
-0.188
-0.010
-0.031
-0.087
-0.007
-0.084
-0.123
-0.065
0.134
0.152
-0.083
-0.055
12




1.000
0.270
0.770
0.802
0.753
0.592
0.801
-0.168
-0.140
-0.121
-0.107
-0.104
-0.109
-0.162
-0.353
-0.340
-0.311
-0.321
-0.312
-0.332
-0.412
-0.123
0.141
0.130
-0.127
-0.117
6





1.000
-0.082
0.021
0.036
-0.019
-0.072
0.095
0.098
0.323
0.368
0.285
0.174
0.420
0.052
0.357
0.439
0.516
0.492
0.375
0.551
0.323
0.421
0.523
0.533
0.333
0.521
-0.036
-0.233
0.212
0.112
-0.238
-0.201
13





1.000
0.449
0.418
0.625
0.810
0.248
-0.038
0.408
0.090
0.076
0.144
0.250
0.008
0.078
-0.309
-0.278
-0.223
-0.109
-0.265
0.197
-0.378
0.444
0.329
-0.415
-0.293
7






1.000
0.562
0.-534
0.696
0.831
0.369
0.875
0.329
0.300
0.522
0.698
0.133
-0.028
-0.085
-0.270
-0.294
-0.242
-0.143
-0.328
-0.271
-0.536
-0.538
-0.494
-0.362
-0.497
0. 152
-0.138
0.147
0.104
-0.146
-0.116
14






1.000
0.987
0.938
0.817
0.923
-0.183
0.305
0.461
0.456
0.458
0.414
0.381
-0.184
0.041
0.077
0.039
-0.032
0.065
-0.385
-0.528
0.612
0.476
-0.573
-0.425
                Leveler Bar Study
Correlation Matrix for Full Model - Heat-up Data
                       248

-------
                                TABLE 27  (continued)
15  FINAL TEMP 3
16  FINAL TEMP 5
17  FINAL TEMP 6
18  FINAL Itnt- I
19  COOL TIME
?0  DELTA TEMP I
21  DELTA TEMP 2
22  DELTA TEMP 3
23  OELTA TEMP 5
24  DELTA TEMP 6
25  DELTA TEMP 7
?6  RATE TEMP. RISE I
27  RATE TEMP. RISE 2
28  RATE TEMP. RISE 3
29  RATE TEMP. RISE 5
30  RATE TEMP. RISE 6
31  RATE TEMP. RISE 7
32  STROKES/MIN
33  INVERSE TIME
34  ROOT TIME
35  SCR TIME
36  INVERSE ROOT TIME
37  INVERSE SQR TIME
22  DELTA TEMP 3
23  DELTA TEMP 5
24  HELTA TEMP 6
25  DELTA TEMP 7
26  RATE TEMP. RISE 1
27  RATE TEMP. RISE 2
28  RATE TEMP. RISE 3
29  RATE TEMP. RISE 5
30  RATE TEMP. RISE 6
31  RATE TEMP. RISE 7
32  STROKES/MIN
33  INVERSE TIME
34  ROOT TIME
35  SOR TIME
36  INVERSE ROOT TIME
37  INVERSE SOR TIME
29  RATE TEMP. RISE 5
30  RATE TEMP. RISE 6
31  KATE TEMP. RISE 7
32  STROKES/MIN
33  INVERSE TIME
34  ROOT TIME
35  SCR TIME
36  INVERSE ROOT TIME
37  INVERSE SOR TIME
36  INVERSE ROOT TIME
37  INVERSE SQR TIME
15
1.000
0.938
0.798
U . fl o
•0.191
0.294
0.423
0.445
0.446
0.395
0.374
-0.161
0.025
0.089
0.060
-0.019
0.068
-0.395
•0.475
0.559
0.448
•0.517
•0.383
22
1.000
0.966
0.858
0.950
0.295
0.702
0.768
0.705
0.516
0.722
•0.152
•0.596
0.697
0.519
•0.655
•0.459
29
1.000
0.729
0.810
0.114
•0.190
0.147
0.018
•0.195
•0.144
36
1.000
0.893
16
1.000
0.918
u . ou r
-0.170
0.303
0.300
0.313
0.365
0.354
0.213
-0.152
-0.138
-0.079
-0.053
-0.084
-0.112
-0.209
-0.470
0.554
0.450
-0.512
-0.377
23

1.000
0.904
0.877
0.317
0.629
0.697
0.717
0.540
0.626
-0.074
-0.622
0.741
0.578
-0.686
-0.477
30

1.000
0.533
0.166
-0.128
0.138
0.043
-0.146
-0.074
37

1.000
17

1 . CCO

-0.145
0.351
0.247
0.243
0.308
0.397
0.140
-0.128
-0.232
-0.185
-0.149
-0.043
-0.200
-0.133
-0.489
0.585
0.461
-0.537
-0.387
24


1.000
0.740
0.333
0.475
0.546
0.573
0.697
0.463
-0.014
-0.591
0.749
0.593
-0.667
-0.437
31


l.OCO
-0.121
-0.240
0.175
0.044
-0.234
-0.226



18



-0.174
0.260
0.453
0.480
0.438
0.351
0.461
-0.146
0.140
0.195
0.125
-0.000
0.210
-0.482
-0.417
0.481
0.380
-0.451
-0.345
25



1.000
0.283
0.735
0.783
0.683
0.463
0.839
-0.185
-0.506
0.584
0.433
-0..554
-0.396
32



1.000
0.303
-0.208
-0.130
0.275
0.346



19



1.000
-0.025
-0.092
-0.103
-0.087
-0.078
-0.038
0.154
0.006
-0.012
0.033
0.041
0.039
0.089
0.101
-0.103
-0.065
0.105
0.094
26




1.000
0.421
0.469
0.561
0.539
0.368
0.385
0.045
-0.015
-0.043
0.027
0.092
33




1.000
-0.835
-0.461
0.985
0.955



20




1.000
0.696
0.711
0.753
0.784
0.636
0.672
0.375
0.443
0.474
0.459
0.392
0.118
-0.517
0.637
0.482
-0.579
-0.384
27





1.000
0.957
0.884
0.608
0.901
-0.016
-0.174
0.125
-0.005
-0. 176
-0.139
34





1.000
0.836
-0.913
-0.671



21





1. 000
0.977
0.947
0.843
0.927
0.254
0.718
0.729
0.665
0.479
0.699
-0. 154
-0.631
0.731
0.534
-0.693
-0.488
28






1.000
0.933
0.659
0.920
-0.031
-0.221
0.170
0.029
-0.223
-0.185
35






1.000
-0.573
-0.302



                                      249

-------
                           APPENDIX  D

                           EMISSION DATA

OBSERVATION PROCEDURE

   The basis for evaluation  of charging with respect to emissions
was the Ringelmann code.   This  method was selected since most
government air polLuticn  regulations are based on the Ringlemann
Number or the equivalent  opacity.   The readings of smoke classifica-
tion were defined so that a direct comparison could be made with
the local air polution  control  requirements.  The time of emissions,
classified by opacity  ( TO, Tl,  T2,  T3),  the charging time, and
the charge cycle time were recorded using 5 stop watches mounted
on a multiple timer board.  The recorded parameters are defined
in the glossary.

   The observation was made  at a  distance of approximately
50 feet from the charging car with the observer positioned at
the south end towards the quench tower.   If the wind was coming
from the south, then the  observation was made from the north end
of the car.

RECORDING PROCEDURE

   In recording the various  Ringlemann times,  the principal
source of emissions was noted by giving the charging hole number
(between ring and drop  sleeve),  or by noting the hopper (H) if
it leaked through the butterfly valve.  If the T3 emissions
exceeded #3 Ringlemann, this  was noted.

   The steam pressure  and temperature were read at the 4" header.
A "high" ascension pipe represented one of the new design  "C"
goosenecks while "low"  represents  the existing design "A" type.
In evaluating the condition of  the ascension pipe, the upper
portion of data sheet represents the gooseneck condition, and
the lower part represents the standpipe.

   The charging hole data  indicates (at left side) proper seat-
ing of drop sleeve if "OK"  is noted.  The data on the right
represents the flare carbon condition.  The comments for the lid
                              250

-------
OBSERVATION PROCEDURE  (continued)

represent the quantity of smoke leakage,  and  also  how long  it took
to seal.  The general comments usually  indicate  the  gap between
the drop sleeve and the charging hole ring, if the seating  was
not proper before start of the charge.

DATA SHEETS

    The following data sheets are attached.

    1.  Results of charging 19 ovens on 1-29-73

    2.  Results of charging 10 ovens on 12-13-73  (corresponds
        to data in table  3) including stop watch event data.

    3.  Results of charging 10 ovens on 1-10-74 with  8.3% moisture
        (corresponds to data in table 4)  including stop watch
        event data.

    4.  Results of charging over 1-1 or 1-2 during February 1974
        using jumper pipes (corresponds to part of data shown in
        table 5) including stop watch event data.
                              251

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Recorder
       CHARGING CYCLE OVEN EMISSION DATA SHEET

SZCZEPANSKI	    Date     1-29-73
Time Start
                     10:52
                     11:03
Time Finish

  11:12
                                                          11:23
                                                          11:46
Ringelmann
Time Factor
                         Oven Number
        3-23 M    |   1-25 M   |  2-25 M    |  3-25 M    [  1-27 M
                           Time                      /
TU
Tl
T2
mo

Principal Source
of Emissions
Charging
Time
Charg Cycle
Time
Steam
Pressure
Steam
Temperature
Type Ascension
Pipe
Condition of
Ascension Pipe
Oven Port Seals
#1 Charging
Hole
#2 Charging
Hoi P
#3 Charging
Hole
Ascension Pipe
Lid
Smoke Seal and
Leveler Door
Gen ' 1 . Comments
on Oven Seals
Drop Sleeve
Seating
14
2:00/#2S[3H

.47 #2 & 3H
/Over 3*
#2 and 3
Hopper
2.-15
3:01
134
500
High
Norm
Norm.

/Light
/Med.
3K/
' Heavy
OK
P-4

*2 SRl/2 in
28
1:594l&2 H

:25/#2 H
trnder 3
#2 Hopper
2:12
2:52
134
500
Low
Const.
Norm

OK
/Med.
OK/
X HEAVY
OK/
/ Med.
Light
5 Min.
P-4


57
1:25/
/#1&2&3E

:46X#2 & 3 H
tinder 3
#2 and 3
Hopper
2:22
3:08
134
500
Low
Norm
Norm

OK/
'X Heavy
OK/
'Med. Heavy
OK/ Light
Light
5 Min.
P-4


12
1:52,
# 2 & 3
:25/
#3 H
:18, 1 & 2H
'Over 3*
#1 and 2
Hopper
2:04
2:47
134
500
High
Norm
Const

OK/
X Heavy
OK,
/X HEavy
/ Med.
OK
P-4
#3 DR
1 1/2 in

7
2:46
42 & 3 H
:02/
#3 H
:11/ #2 & 3H
Over 3*
#2 & 3
Hopper
2:19
3:06
134
500
Low
Const.
Norm

OK /
X Heavy
OK/
Med . Heavy
OK/
' Med.
Med.
5 To'lOMin.
P-4


                    * #2 & 3,
                     While
                     lidding
                     #1 & #2
                     #2 & 3
                     While
                     lidding
                     #1 & #2
  While       While       While
  lidding     lidding     lidding
  #1 & #2 H  ' #1 & #2 H  ' #1 & #2 H
                                        252

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CHARGING  CYCLE OVEN EMISSION DATA SHEET
Recorder Szczepanski
Time Start
11:55
Ringplmann
Timp Factor 1 2-27 M
Date
Time Finish
1:10 1:19 1:31
Oven Time
| 3-2 M | 1-4 . | 2-4


1:46

I 3-4
                     Time
TO
Tl
T2
T3

Principal Source
of Emissions
Charging
Time
Charg Cycle
Time
Steam
Pressure
Steam
Temperature
Type Ascension
Pipe
Condition of
Ascension Pipe
Oven Port Seals
#1 Charging
Hole
#2 Charging
Hnlp
#3 Charging
Hole
Ascension Pipe
Lid
Smoke Seal and
Leveler Door
Gen ' 1 . Comments
on Oven Seals


43
1:39/
#2 & 3
:13,
#2
=16/ #2
Over 3*
#2 H
2:10
2:51
134
500
Low
Norm
Norm

OK/
Med.Heav^
OK/
Heavy
/
Light
Light
5 Min.
P-4
Ik in
#3 RS

while
Lidding
#1 & 2 H
10
1:40/
#1-2-3 E
:29,
#2
:51/ #l-2-3E
Over 3*
#3H
2:20
3:10
134
500
Low
Norm
Norm

OK/
X Heavy
OK/
XX Heavy
/
Med.
Med.
5 to 10 Min
P-4
#3 RS 1 in.

#3 Ran
Empty also
while lidd-
ing 1-2-3
16
2:44/
#2 & 3
:51,
#2H
:53/ #2H
Over 3*
#2 H
2:50
4:44
134
500
Low



OK/
Heavy
OK/
X Heavy
3K
XX Heavy
Med.
• 5 Min.
P-4


#2 Ran Empt}
also while
, lidding
#1 & 2H
27
1:03/
#1 & 3
:15 /
#1
=54/ #3
Over 3*
#3 H
1:48
2:39
1-34
500
Low
Norm
Norm
.
OK/
' Med.
OK/
X Heavy
0K/
Heavy
OK
P-4
#3 RS l*s in.

f *#3 Ran
Empty
45
1:03/
#1 & 3
,10,
#2
:51/«
Over 3*

1:58
2:49
134
500
Low
Const.
Norm

OK/
Med.
OK/
Med.
OK/
Light
Heavy
5 to 10 Min
P-4


*#3 Ran
Empty
                       253

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 CHARGING CYCLE OVEN EMISSION DATA SHEET
Recorder Szczepanski
Time Start

Rinaelmann
Time Factor I 1-6
Date
Time Finish
2:07 2:17 2:27
Oven Time
| 2-6 \ 1-6 | 1-8


2:36

I 2-8
                     Time
TO
Tl
T2
T3

Principal Source
of Emissions
Charging
Time
Charg Cycle
Time
Steam
Pressure
Steam
Temperature
Type Ascension
Pipe
Condition of
Ascension Pipe
Oven Port Seals
#1 Charging
Hole
#2 Charging
Hnlo
#3 Charging
Hole
Ascension Pipe
Lid
Smoke Seal and
Leveler Door
Gen1 1. Comments
on Oven Seals

15
2:09,
7#1 & 3

1:32, #3
'Over 3*
#3
3:02
3:56
170
510
Low
Norm
Norm

OK/
XX Heavy
OK/
X Heavy ,
OK/
Heavy
Heavy
5 to 10 Min.
Heavy Smoka^
out of OD.
—

29
1:31,
x#l & 31.
=25/ #1
:55, #2 & 3
'Over 3*
#2
2:10
3:20
170
510
Low
Const.
Norm

OK/
Heavy
OK /
XX Heavy
OK,
Med.
Med.
5 Min.
P-4
1 % on RS
#3

61
2:31 /
7#1 & 3
=48/ #2 * 3
:09, #3H
'Over 3*
#3H
3:51
4:29
170
510
Low
Norm
Const.

OK/
Heavy
OK/
'Med.
OK/
Light
Light
5 to 10 Min.
P-4
#3 RS lin>

63
1:47/ .
#l-2-3H

:35, #3
'Over 3*
#2 & 3H
2:30
3:25
170
510
Low
Norm
—

OK /
X Heavy
OK/
XX Heavy
OK/
Heavy
Light
5 to 10 Min
P-4
#3 RS 1 in.






















* After 80%  While
 also while  lidding
 lidding     #123
 1 2 & 3
While       While
lidding     lidding
   #2       #2 and 3
                     254

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Recorder
       CHARGING CYCLE OVEN EMISSION DATA SHEET

Szczepanski	    Date 	
Time Start
                     2:46
                     2:52
Time Finish 	
  3:06        3:14
                                                                       3:25
Ringelmann
Time Factor
                     1-1U
                                     Oven  Time
                                 2-10
            I    3-10    |  1-12
                                        Time
TO
Tl
T2
T?

Principal Source
of Emissions
Charging
Time
Charg Cycle
Time
Steam
Pressure
Steam
Temperature
Type Ascension
Pipe
Condition of
Ascension Pipe
Oven Port Seals
#1 Charging
Hole
#2 Charging
Knlp
#3 Charging
Hole
Ascension Pipe
Lid
Smoke Seal and
Leveler Door
Gen ' 1 . Comments
on Oven Seals

26
:59/
#2 & 3
1:16
/#2
:21/ #3
/
HnrtPT- ?
#2H
2:12
3:02
170
510
Low
Const.
Norm

OK/
Heavy
OK7
Med.
OK/
Med.
Light
5 Min.
P-4
2 in.RS #3

21
1:52,
#2 & 3
:40
/ #2 & 3
:26/ #2 & 3
TTnrter 3
#2 & 3H
2:32
3:19
170
510
Low
Norm
Norm

OK
Med..
OK ,
XX Heavy
OK/
Med.
Heavy
5 to 10 Min.
P-4
1% in. RS

15
3:05 ,
#2 & 3
:07 #2 when
— / —
*
#2 & 3
2:43
3:27
170
510
Low
Const.
Norm

OK
X Heavy
/
XX Heav
OK/
Med.
Light
5 Min.
P-4
4 in UR #2
Hit Lid

69
1:14,
#1, 3
"/ —
:49 #3
Over 3*
#3
2:16
3:11
170
510
Low
Norm
Norm

0K/
Heavy
OK ,
' X Heavy
/
Med.
Heavy
10 to 15 Min
P-4
#3 UR 1 in.

9
2:23,
#2 & 3
:02
/ #1
:31/ #1
Under 3
#1
2:22
3:05
170
510
Low
Norm
Norm

OK
Med.
OK .
Med.
/
Med.
Light
5 Min.
P-4
1*5 in. RS

                                             #2 Lite
                                               OFF
                                              While
                                              lidding
                                               #1 & 2
                                        255

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                  CHARGING CYCLE OVEN EMISSION DATA SHEET

Weather
Conditions
Ambient
Temperature
Atmospheric
Condition
Wind Velocity
and Direction
Atmospheric
Pressure
Precipitation
Humidity

Weight Per
Cubic Foot
% Volatile
Matter
Moisture
% Fixed
Carbon
Ash
°/=
Sulfur
Oil
Pints/ton coal
Date January 29, 1973


30°
OVER CAST
N N W 6 mph.
29.62
SNOW SHOWERS
84%
Daily Coal Analysis (Lab Record)
43.10
32.26
7.00
59.89
7.85
1.22
3.38
Comments on Data:  (includes equipment malfunctions)




Conclusions:
                                       256

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                  CHARGING  CYCLE  OVEN EMISSION  DATA SHEET
Recorder   John DeFrances

Time Start  1:30     	
                                                 Date
              12-13-73
Time Finish  3: 30
Ringelmann
Time Factor
Tn
*0
TI
T2
T3
Principal Source of
Emis sions
Charging
Time
Charge Cycle
Time
Steam
Pressure
Steam
Temperature
Type Ascension
Pipe
Condition of
Ascension Pipe
Oven Port Seals
#1 Charging
Hole
#2 Charging
Hole
#3 Charging
Hole
Ascension Pipe
Lid
Smoke Seal and
Levcler Door
Gen'l Comments
on Oven Seals

3-9

63
90
89
0

174
242
125

Low

Oven Number
1-11 | 2-11
Time
71
63
49
37*

105
220
125

Low


OK/
Lite
OK/
Lite
OK/
Med.
Lite - 5'
P-4

OK/ .
Lite
OK/
Lite
OK/
Lite
Med. -10'
P-4


74
54
141
30

168
299
125

Low


3-11

92
126
39
15

147
272
125

Low


OK/
Med.
OK/
Med.
OK/
Lite

P-4

OK/
'Lite
OK/
Lite
OK/
Lite
Lite 5'
P-4

1-13

44
95
37
84*

155
260
125

Low


OK/ .
Lite
OK/
Med.
OK/
Lite
Lite 5-10'
P-4

  *  T3 Emissions exceeded #3 part of the  time.
  Charge cycle time recorded as ending with  the lid on #3 charging hole
                                    257

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                  CHARGING CYCLE OVEN  EMISSION  DATA  SHEET




Recorder John DeFrances                         Date   12-13-73
Time Start
           1:30
Time Finish  3 : 30
Ringelmann
Time Factor
Tn

T!
T2
T3
Principal Source of
Emis sions
Charging
Time
Charge Cycle
Time
Steam
Pressure
Steam
Temperature
Type Ascension
Pipe
Condition of
Ascension Pipe
Oven Port Seals
#1 Charging
Hole
#2 Charging
Hole
#3 Charging
Hole
Ascension Pipe
Lid
Smoke Seal and
Leveler Door
Gen'l Comments
on Oven Seals

2-13
Oven Number
3-13
Time
21
124
43
104*

174
292
125

Low

35
125
66
39*

171
265
125

Low


OK/
Lite
OK/
Med. .
OK/M.Hvy.
Lite 5-10'
P-3

OK/
Med.
OK/
Med.
OK/Med.
Med. 5-10'
P-3

1-15
2-15 1 3-15

87
99
176
34*

270
396
125

Low

68
86
91
50*

162
295
125

Low


OK/
Med.
OK/
Lite
OK/M.Hvy.
Lite 5-10'
P-3
Coal Wound
run out #3
TTi'iliiB^I'
OK/
Lite
OK/
Med.
OK/Lite
Med. 10-15
P-3
rt
25
62
96
37*

.114
220
125

Low


OK/
Med.
OK/
Hvy.
OK/Med.
__
P-3

  *  T3 -Emissions exceeded #3  part of the time.
                                    258

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                 CHARGING CYCLE OVEN EMISSION. DATA SHEET
RECORDER
             J.  H. S'toltZ
                                      DATE
12-13-73
Oven No.
Time Start Charge

Time Reach
80% Empty

Hopper
1
2
3
Time Start Level
Time Open
Butterflies
Time. Hopper
Empty
Hopper
1
2
3
Hopper
1
2
3
Time Request Stop
tevel and Close Chuck
Door
Time Chuck
Door Closed
Time Start
Relid
Time Steam
Hopper
1
2
3
Off
Did Swab go in
Dooseneck
% Open Standpipe
complete damper off
Comments start coal fill
coal fill done
Start clean <3,N.of next
oven
Spot car next oven tochc
3-9
1:40
1.0
0.95
1.05
1.05
1.15
1.15
1.15
1.5'
1.7
1.9
2.35
3.3
3.2
3.6
3.85
4.25
NO
80%
4.90
6.20
6.90
7.50
8.40
1-11
1:49
1.05
0.90
1.00-
1.0
1.10
1.10
1.10
1.4
1.75
1.7
2.25
2.90
2.95
3.20
3.45
4.0
YES
70%
4.60
5.40
6.30
7.0
8.1
2-11
1:58
Iil5
0.95
1.85
1.0
1.9
1.9
1..9
2'. 35
2.5
2.8
3.2
4.2
4.25
4.45
4.65
5.1
YES
90%
5.8
7.3
8.1
9.1
9.8
3-11
itir?8l&2
IDsac. Jate
1.03
1.2
1.7
1.05
1.75
1.75
1.75
2.1
2.45
2.45
3.0
4.0
3.75
4.0
4.30
4.7
NO
100%
5.35
6.4
7.3
7.8
8.5
1-13
Approx .
2:17 Times
start #1,2 0.25
min. later
1.35
1.2
1.15
-1.2
1.4
1.4
1.4
1.8
2.35
1.95
2.8
3.6
3.65
3.85
4.10
4.55
YES
75%
5.5
6.3
7.2
8.1
9.2
                                      259

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RECORDER
     CHARGING CYCLE OVEN . EMISSION. DATft SHEET





J. H. Stoltz	    DATE   12-13-73
                       USES P-3 PUSHER MANUAL LEVEL
Oven No.
Time Start

Time Reach
80>o Empty

Tine Start
Time Open
Butterflies
Tim!? Hopper
Empty
Charge
Hopper
1
2
3
Level
Hopper
1
2
3
Kcpper
1
2
3
Time Request Stop
Level and Close Chuck
Door
Time Chuck
Door Closed
Time Start
Relid
Time Steam
Hopper
1
2
3
Off
Did Swab go in
Gooseneck
% open stand pipe
Complete damper off
Comments Start coal fill
Coal fill done
Start cln.G.N.of nextoven
Spot car next oven to
chg.
	
2-13
2:37
start #1,2
15 see later
1.25
1.05
1.20
1.0
1.25
1.25
1.25
1.9
2.4
2.9
3.4
4.5
4.1
4.25 .
4.7
5.0
YES
80%
5.6
6.65
7.6
8.65
9.45
3-13
2:47
start #1,
15 sac later
1.45
1.2
1.1
1.15
1.45
1.45
1.45
2.85
1.8
2.85
3.3
4.75
4.0
4.2
4.4
4.75
NO
50%
5.5
6.8
8.15
9.0
9.5
T 	 	 	
1-15
2:58
start #1,2
15 sec later
1.4
1.3
3..0
1.3
3.0
3.0
3.0
3.2
3.5
4.5
4.5
5.2
6.0
6.2
6.4
6.75
YES
50%
/.4
8.2
9.0
9.8
10.2
	 : 	 1
2-15
3:07
0.60 min.
]starstai±l&2
1.8
1.5
1.7
1.5
1.8
1.8
1.8
2.2
2.7
2.6
3.2
4.1
4.1
4.4
4.7
5.0
YES
85%
" b . 6
6.5
7.2
8.5
9.3
3-15
3:17 Approx.
Times
.0 sec, later
start 1,2
1.1
1.0
1.05
1.05
1.1
1.1
1.1
1.5
1.9
1.6
2.4
3.3
3.0
3.2
3.4
3.7
YES
70%
Not recorded
Not recorded
Not recorded
                                     260

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                     CHARGING CYCLE OVEN EMISSION DATA SHEET
                                                        Date   12-13-73
Weather
Conditions
Ambient
Temperature
Atmospheric
Condition
Wind Velocity
and Direction
Atmospheric
Pressure
Precipitation
Humidity

41°F
Overcast - Had been raining just previous to taking test data
S . E . 5 mph
29.14
None
85%
Daily Coal Analysis (Lab Record)
Weight Per
Cubic Foot
% Volatile
Matter
%
Moisture
% Fixed
Carbon
%
Ash
%
Sulfur
Oil
pints/ton coal
42.78
32.22
7.06
60.91
6.87
1.21
2.5 - 2.9 pints/ton
Comments on Data: (includes equipment malfunctions)
Pulverization % on 3/4" 0%
on 1/2" 1.0
on 1/4" 6.5
on 1/8" 17.7
thru 1/8" 74.8
Conclusions:
                                           261

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                  CHARGING CYCLE OVEN  EMISSION  DATA  SHEET
Recorder    D.  Cipallone
Time Start   11:0°
  Date   1-10-74
                                           Time Finish   12:00
Ringelmann
Time Factor
Tn

T!
T2
T3
Principal Source of
Emis sions
Charging
Time
Charge Cycle
Time
Steam
Pressure
Steam
Temperature
Type Ascension
Pipe
Condition of
Ascension Pipe
Oven Port Seals
#1 Charging
Hole
#2 Charging
Hole
#3 Charging
Hole
Ascension Pipe
Lid
Smoke Seal and
Levcler Door
Gen'l Comments
on Oven Seals

2-21

0:13
0:33
0:30
3:12
#3+2 hoppe:
3:45
4:28
118

Low

Oven Number
3-lq
Time
0:04
3:11
0:50
0
: 3+2 hcpper
3:40
4}05
121

High


Med . /OK
Med./OK
Med. /OK
Light 5-10
4 puslier

Med./OK
Med./OK
Med./
over
Heavy 30
4 pusher
#3 Drop Slv
4" off
"}— 91

0:03
2:13
0:50
2:09
3+2 hqcper
4:02
5:15
121

High

1-23
2-2^

0:43
1:41
0:36
0:03
3 +2 hcpper
2:30
3:03
118

LOW


Med./OK
Heayi/OK
Light/OK
over
Heavy 30
4 pusher

Med./OK
Light/OK
Liqht/
over
Heavy 30
4 pusher
f!v?i?S I-
1:15
0:17
0:49
0:42
3+2hqpper
2:20
3:03
118

Low


Med/OK
Med./OK
Licrht/OK
over
Heavy 30
4 pusher

                        WE 1:15   Fire  1:05
                        Fire 2:28
                        #7 Hop.
WE 3:55   Fire 0:30  WE 2:10.
                                    262

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                  CHARGING CYCLE OVEN EMISSION DATA SHEET
Recorder  D.  Cipallone
      Date
              1-10-74
Time Start   2:0°
Time Finish   2:15
Ringelmann
Time Factor
Tn
A0
T!
T2
T3
Principal Source of
Emis sions
Charging
Time
Charge Cycle
Time
Steam
Pressure
Steam
Temperature
Type Ascension
Pipe
Condition of
Ascension Pipe
Oven Port Seals
#1 Charging
Hole
#2 Charging
Hole
#3 Charging
Hole
Ascension Pipe
Lid
Smoke Seal and
Levcler Door
Gen'l Comments
on Oven Seals
Oven Number
3-23

1:33
0:29
0:27
0:51
3+2 hopper
2:50
3:20
128

High

1-27
Time
2:29
1:17
0:22
0:04
3 hopper
3:20
4:12
116

Low


Med./
OK
Med./
OK
Light/
IK
Med. 20
#4 Pusher

Med./
OK
Light/
OK
Light/
Medium
#4 Pusher
3 Drop slv
off 4"
2-2
1-4
2-4

2:19
1:02
0:32
0:02

2. -50
3:55
116

Low

0:17
1:56
0:46
0:56
3+2 hopper
2:47
3:55
144

Low


Med./
OK
Light/
• OK
Light/
OK
Extra
Heavy
#4 Pusher

Med./
Light/
Light/
Heavy
#4 Pusher
#2 hopper
off 3"
2:45
1:10
0:42
0:35

4:15
5:12
114

Low


Light/
OK
Heavy/
OK
Heavy/
OK
Heavy
#4 Pusher

                                  #2:25  fire
                                                         WE 2:40
                                       263

-------
RECORDER
  CHARGING CYCLE OVEN EMISSION. DATA SHEET





-Szczepanski	     DATE     1-10-74
                          COAL  VERY  WET
Oven No.
Time Start

Time Reach
80>o Empty

Charge
Hopper
1
2
3
Time Start Level
Time Open
Butterflies
Time Hopper
Empty
Hopper
1
2
3
Hopper
1
2
3
Time Request Stop
level and Close Chuck
Door
Time Chuck
Door Closed
Time Start
.Relid
Time Steam
Hopper
1
2
3
Off
Did Swab go in
Gooseneck
Comments
2-21
11 00
2:43
2:23
2:26
2:25
Ran
Contin.
—
3:00
3:21
3:00
4:00
4:40
3:45
3:56
	 4^10

YES
Poke 1
shut off
2 & 3
until top
It. of 1
came on
3-19
11:10
2:24
2:00
1:52
2:07
2:37
. 2i37
—
2:50
3:20
2:24
3:50
4:23 '
3:40
3:50
4:03

YES
Poke 1&2
shut off
.3 until
1 & 2
te jamb ,
near end
3-21
11:19
2:10
1:48
1:40
1:52
2:16
2:16

2:36
3:57
2:24
5:00
5:30
4:25
5:00
4:15

YES
Poke 1 & 2
#2 jamb
backed up
in hole
.
1-23
11:31
1:24
1:14
1:07
1:25
1:40
1:40
—
1:53
2:09
1:35
2:42
5:20
2:28
2:40
2:53

YES

2-23
11:39
1:10
51
55
1:00
1:20
1:20
	
1:40
2:03
1:28
2:30
3:02
2:20
2:30
2:45

YES

                                      264

-------
RECORDER
  CHARGING CYCLE OVEN EMISSION. DATft SHEET





Szczepanski	    DATE   1-10-74	
Oven No.
Time Start Charge

Time Reach
30% Empty

Hopper
1
2
3
Time Start Level
Time Open
Butterflies
Time Hopper
Empty
Hopper
1
2
3
Hopper
1
2
3
Time Request Stop
Level and Close Chuck.
Door
Time Chuck
Door Closed
Time Start
Re lid
Time Steam
Hopper
1
2
3
Off
Did Swab go in
Gooseneck
Comments
3-23
11:47
2:00
1:37
1:34
1:45
2:11
2:11
_
2:28
2:37
2:10
3:14
3:51
2:54
3:05
3:16

YES
Poke 1
1-27
1:17
2:20
2:00
1:56'
2:05
2:28
2:28
_
2:43
3:00
2:27
3:24
3:58
3:30
3:40
3:58

YES
Poke 1& 2
#1 Lid
d id not
go on
2-2
1:37
2;07
1:56
2:04
2:11
2:22
2:22
_
2:30
2:52
2:37
3:25
4:05
3:07
3:25
3:35

YES

1-4
1:51
2:02
1:56
2:02
2:02
2:19
2:19
_
2:31
2:42
2:31
3:15
3:55
2 ;54
3:04
3:40

YES
i
2-4
2:02
2:13
2:00
2:01
.2:00
2:20
2:20
-
2:35
4
2:42
4:25
5:04





Poke 2
                                     265

-------
                     CHARGING CYCLE OVEN EMISSION DATA SHEET

                                                        Date  1-10-74
Weather
Conditions
Ambient
Temperature
Atmospheric
Condition
Wind Velocity
and Direction
Atmospheric
Pressure
Precipitation
Humidity

35°F
Over Cast
From N. - N.E. 5 mph
29.97
Intermittent Rain
89%
Daily Coal Analysis (Lab Record)
Weight Per
Cubic Foot
% Volatile
Matter
%
Moisture
% Fixed
Carbon
%
Ash
%
Sulfur
Oil
pints /ton coal
41.49
32.22
9.26%
60.44%
7 . 34%
1.21

Comments on Data: (includes equipment malfunctions)
      Pulverization
Conclusions:
                                           266

-------
                  CHARGING CYCLE OVEN  EMISSION  DATA SHEET
Recorder
            D. Cipollone
      1-10-74 to
Date  2-22-74
Time Start
                        	     Time Finish

                         1-10-74   2-14-74    2-15-74
                                                          2-21-74
                                                                     2-22-74
Ringelmann
Time Factor
Tn
*0
T!
Tz
T3
Principal Source of
Emis sions
Charging
Time
Charge Cycle
Time
Steam
Pressure
Ste'am
Temperature *
Type Ascension
Pipe
Condition of
Ascension Pipe
Oven Port Seals
#1 Charging
Hole
#2 Charging
Hole
#3 Charging'
Hole
Ascension Pipe
Lid
Smoke Seal and
Levcler Door
Gen'l Comments
on Oven Seals
Oven Number
1-2

3:36
0:21
0:06
0 :04
3 hopper
3:00
4:07
'109
_
Low
•>
1-2
Time
3:04
0:14
0
0 :02

2:45
3:20
125
_
Low
100%

OK/
Med.
OK/
Med.
No/
Light .
Heavy
#4 Pusher
used
#3 Drop
slv.of f
OK
Med.
OK/
Med.
OK
Med.
Med.
5 min.
#4
--
l_l

3:45
0:08
0
0 :02
#1 hopper
D 1:55
2:30
3:35
127 .'
_
Low
95% •'
1-2
1-1

3 : 14
0:08
0
0 :03
#2 & #3
2:18
. ,3:25
116
_ i
Low.
95%

OK/
Light
OK/
Med.
OK/
Med.
Light
#4
i-ire #2
hopper @
ok/
Med.
OK/
Med.
OK/ ,,, *
Med.:'
Light
#4
Emissions
at
2:57
0:07
0
.0 :02
#1 & #2
2:21
3:06
'. 130
—
Low
95%

OK/
Med.
OK/
Hvy.
OK/ .
Light
Light
#4
Emissions
at
                       nole  for
                       25 seconds
                                               2:05"      x:uu2sec.1:50 6 sec.
                                                         1:40 2 sec. 2:05 1 se'c.
                                                         1:58 4 sec.
 *  Approximately 450°F
                                           267

-------
RECORDER
     CHARGING CYCLE OVEN  EMISSION. DATft SHEET




Szczepanski               DATE   1-10-74 to 2-22-74
Oven No.
Time Start Charge

Time Reach
80% Empty

Time Start
Time Open
Butterflies
Time Hopper
Empty
Hopper
1
2
3
Level
Hopper
1
2
3
Hopper
1
2
3
Time Request Stop
Level and- Close Chuck
Door
Time Chuck
Door Closed
Time Start
Relid
Time Steam
Hopper
1
2
3
Of*\
Did Swab go in
Cooseneck
Comments
1-10-74
1-2
(1:29 pm)
0
1:45
1:45
1:40
1:45
2:20
2:20
—
3:00
3:10
3 :00
3:50
4:40
3:45
3:15
3:35
—
Yes
Poke #2
Drop slv.
2-J4-74
1-2
0
p
1:00
1:05
1:10
1:15
1,15
.1:15
2:55
2:10
2:15

3:00
3:05
2:15
2:-45


#1 Butter-
fly jamm-
ed
2-15-74
1-1
Started 2
after top
level, lite on
for #1
1:15
1:15
1:10
1:20
1:25
1:25
1:25
2:15
2:30
2:35

3:15
3:20
2:45
3:20


Top Level
lites show
coal has
started -out
of hopper
.
2-21-74
1-2
Timing Dat
Relidded i
Holes Pric
Leveler DC

















2-22-74
Irl
a not Taken.
11 Charging
r to the
or being Shut.

















                                     268

-------
Recorder
                  CHARGING  CYCLE  OVEN. EMISSION  DATA SHEET
             D. Cipottone
             Date
           3-5-74 to
           3-25-74
Time Start
                         3-5-74
	    Time Finish

 3-6-74    3-15-74
                                                            3-18-74    3-25-74
Ringelmann
Time Factor
Tn
*0
T!
Tz
T3
Principal Source of
Emis sions
Charging
Time
Charge Cycle
Time
Steam
Pressure
fi. _ _. 	 .
Ott^ri.t*
Temperature
Type Ascension
Pipe
Condition of
Ascension Pipe
Oven Port Seals
#1 Charging
Hole
#2 Charging
Hole
#3 Charging
Hole
Ascension Pipe
Lid
Smoke Seal and
Levolor Door
Gcn'l Comments
on Oven Seals
Oven Number
1-1

3:39
0:02
0:00
0:04
#1,#3
Sleeve
2:30
3:45
124

Low
80%
1-2
1-1
1-1
1-2
Time
3:11
0:04
0:00
0:05
#1, #2
Sleeve
2:29
3:20
140

Low
95%

Med/OK
Hvy/OK
Med/OK
Light
#4 Pusher

Med/OK
Med/OK
Med/OK
Light
#4 Pusher
1:15 #1
1 :50 #1
1:49
0:05
0:12
0:09
#1, #3
D. Sleeve
1:50
2:20
136 .

Low
85%
3:53
0:06
0:07
0:03
#2 Sleeve
3:45
4:09
132

Low
80%

Med/OK
Bvy/OK
Med/OK
Light
#4 Pusher
0:30 #1
10:05 #3
Med/OK
Med/OK
Med/OK
Light
#4 Pusher
0:10) #1,3
0:15) Sleeve
3:05
0:07
0:03

#2 Drop
Sleeve
2:05
2:45
130

Low
100%

Med/OK
Med/OK
Med/OK
Heavy
#4 Pusher
T-L + T2 #2 D. S
1:30
     #1
2:15 #2
1:50 #1
                      2:15  #2
                                                                     T]_ #2 D.S.
                                                                     2:00
                                         269

-------
RECORDER
   CHARGING  CYCLE OVEN EMISSION DATA SHEET




Szczepanski	    DATE   3-5-74 to 3-25-74
Oven No.
Time Start Charge

Time Reach
80% Empty

Time Start
Time Open
Butterflies
Time Hopper
Empty
Hopper
1
2
3
Level
Hopper
1
2
3
Hopper
1
* 2
3
Time Request Stop
Level and Close Chuck
Door
Time Chuck
Door Closed
Time Start
Relid
Time Steam
Hopper
1
2
3
Off
Did Swab go in
Gooseneck
Comments
3-5-74
1-1
0
1:05
0:55
1:15
1:25
1:35
1:35
1:35
2:03
2:04
2:05

3:00
3:00
3:10
3:35



3-6-74
1-2
0
1:00
1:00
1:05
1:05
1:35
1:35
1:35
2:20
2:00
2:03


2:30
2:40
2:55



3-15-74
1-1
0
1:00
1:08
1:00
1:00
1:30
1:30
1:30
1:51
1:46
1:51


1:55
2:05
2:15



3-18-74
1-1
0
1:00
1:00
1:15
1:00
1:45
2:30
3:10
2:10
2:55
3 .40


2:15
3:00
3:50



3-25-74
1-2
0
1:00
0:55
0:55
1:00
1:20
1:20
1:20
1:55
1:50
1:45
1
2:35
2:05
2:10
2:15



                                      270

-------
Daily Coal Analysis
Date
1-10
2-14
2-15
2-21
2-22
3-5
3-6
3-15
3-18
3-25
WT/FT3
41.49
39.86
42.71
42.99
43.40
41.66
39.58
41.85
42.36
42.08
Vol.
% Matter
32.22
32.28
32.28
32.27
32.26
32.26
32.23
32.26
32.23
32.24
o/
/a
Moisture
8.26
8.09
7.55
8.50
8.03
7.56
8.00
8.49
8.00
8.54
o/
/o
Fixed
Carbon
60.44
60.38
60.35
60.48
60.56
60.63
60.39
60 . 65
60.45
60.51
% Ash
7.34
7.18
7.27
7.25
7.18
7.11
7.38
7.09
7.33
7,25
OH.PTS/
Ion Coal
2.69
1.20
1.20
1.81
2.50
2.43
1.87
p
?
2.44
       271

-------
                            APPENDIX E

                         EMPTY OVEN TESTS

   The procedure  used to estimate the ascension pipe gas flow
as a  function of steam ejector thrust and steam pressure was fully
described  in a  previous report on this work9.  That procedure
is outlined here.   The test arrangement is shown on Figure 50 (pg.157)
Details of the  special orifice flow meter are shown in Figure 75.

   In the test work on P-4 battery high pressure, super heated
steam (200 psig, 500°F)  was supplied from an auxiliary 4" header.
A 1"  line  connected the steam nozzle to the 4" header.  A pressure
regulator  was connected in the 1" line near the header.

   A test run  consisted of taking vacuum measurements with
different  size  steam nozzles at different steam pressures.  The
values of  oven  vacuum, flow meter differential pressure, steam
pressure,  and steam temperature recorded during the test were
used  to calculate the nozzle and air flow rates. The method of best
fit was used  to determine the performance curves for each trial. The
average performance curve was computed using the best fit curve
for each test and  calculating the average values.

   Thrust was  used as the independent variable because it is
a good indication  of input energy.

METHOD OF  CALCULATION

   Mass Flow of Steam

   W = 0.3155 (At)   riT^              From Kent's
     s                                Mechanical Engineers
                                     Handbook - 8 - 18
   Ws =  Pounds  of  superheated steam per second
   At =  Area  of throat - In.2
   P! =  Initial pressure - PSIA

   V^ =  Specific volume - Ft.3/lb. at P-^ and T-
                               272

-------
^^
    B-
 l.D.  , ,.
    g-2
 273

-------
METHOD OF CALCULATION (continued)
   Nozzle Thrust
    F = Pt At
                   V
                     From: Elements of Fluid
                     Mechanics by D.G.Shepherd ,
                     1965. Harcourt, Brace and
                     World Inc., New York
   Assume: PI and  T-[_  are  stagnation

           values  (V~  = 0)
    Pfc =  Pressure  at  the throat = 0.55 P^ - PSIA
                              o
    At =  Area of throat  - In.
    Ws =  Flow of steam - Ib/sec.

    gc =  Constant  =32.2

    HI =  Enthalpy  at  initial conditions

    H. =  Enthalpy  at  the throat conditions
          (This value  is  taken from a Mollier Chart)

    Vfc =  Velocity  of  steam at the throat
                       -  Ht(T78.3)  Ft/Sec .
   Air Flow Rate

   Q =  C  • D2  .
Hi - P
M • B ' X  From: Flow Meter
           Engineering
           Handbook by the
           Brown Insititute  Co.
                              274

-------
METHOD OF CALCULATION  (continued)

    Air Flow Rate  (continued)

    Q =  Air Flow Rate - Ft. /hr. at 30" Hg, 60°F, dry gas

    C =  Orifice coefficient of discharge - 0.76

    D =  Pipe diameter = 10.0 inches
    H =  Differential pressure across the orifice
    H-^ = Differential pressure factor - VH~

    PO = Atmospheric pressure - 30" Hg

    P =  Gas pressure factor - 237.1 >fPQ  = 1298.6

    t =  Operating temp. °F
    T =  Gas temperature factor = V519.63/(459.63 + t)

    S =  Specific gravity factor = 1.0

    M =  Moisture factor = 1.0

    B =  Gas base factor - 1.0
    X =  Flow meter correction factor based on calibration done
         by the Colorado Engineering Experimental Station -
         = 0.15H +0.54    Up to X= 0.7

TEST PROCEDURE

    The following describes the work required to set up for a
typical test run:

    1.  Charge walkie-talkie batteries the day before the test.

    2.  Notify all required personnel: Operating, Maintenance and
                                       Research.

    3.  Turn the 8 channel recorder on at least one hour prior to
        testing.

                                275

-------
TEST PROCEDURE  (continued)

   4.  Examine the oven  to be  tested  and  clean  the  gooseneck,
       the standpipe and the charging holes  if  necessary.   Clean
       away any carbon near the  steam nozzle connection.

   5.  Make sure oven doors are  tight,  especially the  chuck door.

   6.  Install the first nozzle  to  be tested.

   7.  Install a 1" steam line from the special 4"  header  to the
       gooseneck steam nozzle.  The line  has a  pressure  regulator,
       pressure tap, temperature tap,  pressure  gauge and a quick
       opening valve.

   8.  Install the pressure tap  in  the base  of  the  standpipe.

   9.  Connect the standpipe pressure tap to a  pressure  transducer
       with +2 to -8 inches of E^O  scale  range.
   10.   Install  the  thermocouple  in the base of the  standpipe.

   11.   Connect  the  standpipe  thermocouple  to the. 8  channel
        recorder (500  to  2000°F temperature range channel) .

   12.   Connect  the  steam pressure  tap to the 50-200 psi transducer.

   13.   Install  steam  temperature thermocouple.

   14.   Connect  steam  temperature thermocouple to 8  channel
        recorder.

   15.   Install  a  lid  with a pressure tap on the No. 1 charging
        hole  (pusher side) .  Seal lid with refractory cement.

   16.   Connect  the  lid to a pressure transducer with +2 to  -8
        inches of  water scale  range.

   17.   Repeat steps 13 and 14 for  charging hole No. 3 and for
        the smoke  hole.

   18.   Place the  flow meter over #2 charging hole,  sealing  it
        with asbestos  rope between  its bottom flange and the oven.
        Use refractory cement  to  seal it.

                              276

-------
TEST PROCEDURE  (continued)

   19.  Connect the flow meter to one of the differential pressure
        transducers.

   20.  Connect all transducers to the 8 channel recorder.

   21.  Check out all test equipment and calibrate it.  Note the
        weather conditions, the collecting main pressure, and
        ammonia liquor line pressure.

   22.  Run the test using the various steam pressures and nozzle
        sizes required, as described below.

   23.  After completion of the test dismantle the equipment and
        store it in the proper areas.

   24.  Examine recorder chart and take off data.

   25.  Punch out data  cards and make a computer run for
        calculated data.

     After the test apparatus had been set up, the actual test was
run according to the following steps for each steam pressure
setting:

    1.  Set the ejector steam pressure.

    2.  Turn the ejector steam on and open the damper valve.

    3.  Wait for the readings to stabilize with the butterfly
        valve closed in the flow meter.

    4.  Open the butterfly valve and wait until a fairly constant
        differential pressure  across the flow meter orifice is
        recorded.

    5.  Be sure all recorder channels are working properly.

    6.  Close the damper valve, turn off the ejector steam, then
        repeat for the next pressure.

                              277

-------
TEST PROCEDURE  (continued)

   When all pressure settings were used the nozzle was changed
and the above steps were repeated.

TEST EQUIPMENT

guantity                      Description

  1          Smoke hole lid with a pressure tap  (1/2" pipe)

  2          Charging hole lids with pressure  taps  (1/2"pipe)

  1          Pressure tap for the base of  the  standpipe  (1/2"
             pipe)

  1          Thermocouple  (Cromel-Alumel)  for  measuring  the  gas
             temperature  (0-2000°F)  inside of  the  standpipe

  1          Pressure tap for the collecting main

  2          Orifice flow meters PSX-5163  (Custom  designed for
             this application - see Figure 75)

  400  feet   3/8" type L copper tubing  (soft)

  20         Tubing splices 3/8

  8          3/8 tubing to 1/2" pipe male  thread

  8          3/8 tubing to 1/2" pipe female  thread

  10         3/8 tubing to transducer

  1          Thermocouple for measuring  steam  temperature
              (Crome1-Alume1)

  1          Pressure recorder, ±  15 MM  H2O  range

  1          Eight channel oscilliograph recorder

  2          Differential pressure  transducers,  0-50 MM
             H2O  range

                              278

-------
TEST EQUIPMENT (continued)

Quantity                   Description

    5         Pressure transducers, +2" to -8" H~O range

    1         Pressure transducer 50 to 200 psi range

    1         Cart with wheels for eight pressure transducers

    1         Air conditioned (heated and cooled) building
              4'  x 11' x 8' high, with lifting lugs, to store
              recorder etc., on battery

    1         Thermometer                 »   ,.     , .   .
                                          )   for ambient
                 .  .           .      .      )   air conditions
    1         Humidity measuring device   »

    1         Pressure regulator with a pressure gauge, 50-200
              psi range

    10 feet   1"  diameter asbestos rope

    1         Bucket of sealing mud

    3         Steam pressure regulators 25 - 200 psi range

    1         Steam pressure gauge 0-200 psi range

    1         Heise pressure gauge to check steam pressure
              transducer calibration

    1         Potentiometer for thermocouple checks

    1         Manometer

    *         Assorted pipe fittings and lengths of pipe

    2         Walkie-talkies

                               279

-------
                            APPENDIX  F

                 BATTERY DIMENSIONAL VARIATIONS

   The use of a  larry  car for mechanized charging depends on consistent
alignment with individual ovens,and requires an investigation into
the dimensional variations of the battery.   The equipment design
must  include allowance  for these expected variations.

   The battery growth  was determined in a  recent survey taken
at P-4 battery and  is compared with a similar one taken in 1965,
and also the original plan.   It can be seen that the buckstays at
the top of the battery  have been pushed outward from about 2 1/2"
at the ends to as much  as 7 11/16" at the center.  In general
the buckstays at  the north end of battery (coal bin)  tilt in
that  direction as much  as 2 7/8" and those  at the south end of
battery tilt as much as 4 5/16".   This can  be seen in Figure 76.

   A major consideration is to determine the location of the
larry car tracks  on the battery.   On a new  battery the tracks would
be located within a specified tolerance. Limits must be established
for   allowable vertical and horizontal movement that would affect
the position of the larry car with respect  to the standpipe or
charging holes.   On an  existing battery a survey must be made to
determine the position.  In most cases the  rails would require
shimming to provide a stable position from  which to make any
alignment adjustments.   On P-4 battery the  track elevation at the
coal  bin and at the opposite end was significantly higher than on
the main body of  ovens.  The maximum variation in elevation was
measured to be 1  3/8" on the coke side track and 1 1/2" on the
pusher side track.  The deviation of rails  from a longitudinal
centerline  (length  of battery) was _+ 7/8" on the pusher side and
+ 9/16" on the coke side.  One bowed section of rail was replaced
to reduce the variation.  The rails were shimmed to minimize the
vertical movement.  This was also necessary to prevent spalling
of brick under the  rail chairs.  The shims  had a tendency to move,
and required re-work to keep in place.

   A survey of the cross battery position of charging hole rings
with  respect to a longitudinal centerline indicated a band of
2.25" for #1 charging holes, 2.625" for #2, and 2.875" for #3.
The longitudinal  variation of the three charging hole rings with

                               280

-------
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respect to an oven centerline  (cross battery) was a band of 2.375"
with the average being 1.054".  This meant that in some cases
the misalignment of charging holes for an individual oven
exceeded 2".  When referenced to the position of the gooseneck
inspection port two ovens away the deviation could be considerably
greater.  The alignment of charging hole rings was limited by the
amount of exposed charging hole brick work and the exposure of the
charging hole ring to flame.

    The position of the gooseneck inspection port with respect to
an oven reference point varied in an unpredictable manner.  The
gas collecting main is divided into two independent sections.
The growth of battery across the width pushed out the buckstays
which support the collecting main.  The expansion of the buckstay
along the battery did not necessarily match the battery growth in
that direction at all points.  A history of some local hot spots
in the collecting main resulted in its distortion at some points.
The net result is that stand pipes lean in all directions, and
the location of the gooseneck inspection port is unpredictable.
There is little that can be done to correct this situation, and
the equipment must be designed to operate under this set of
conditions.

    A survey was made along the battery of the position of the
gooseneck port from the top of the larry car rail .  The change
in elevation varied over a band of 3 3/4" while the lateral
measurements had a variable range of 4".  Any movement of the rail
could add to this variation.  With accurate positioning of the
larry car (_+ 1/2"), the variation of 2 ovens widths along the
battery with respect to the gooseneck port provided a band of
3 1/2".

    The type of dimensional variations that occur on a battery
place a severe constraint on the design of operating equipment
which depends on the positional relationship of the larry car
to the battery.  The installation of such equipment is very
difficult on an existing battery, and should be avoided if not
necessary.  The incorporation of this type of equipment on new
batteries should be done with care knowing the type of variations
that can occur in future years.

                             283

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                            APPENDIX G

ASCENSION PIPE PARTICULATE SAMPLING

   A key part of  the  charging system involves the use of an
ascension pipe steam ejector system that is capable of delivering
a volume of gas  equal  to that being generated and displaced during
charging.  The increased volume of gas through the ascension pipe
during charging  results from a greater quantity of steam ejected
into the gooseneck.  The increased steam was obtained by increas-
ing the steam nozzle from 1/2" to 3/4",  increasing the steam header
pressure from 100  psi  to 175 psi, and increasing the diameter
of the branch piping from 3/4" to 1 1/4".

   Since other  coke oven batteries,  that use high pressure steam,
have reported an increase in coal carried into the gas collecting
main, tests were started to determine the magnitude of this
problem.  Ammonia  liquor samples were collected at the bottom of
the gas collecting main,  just downstream from the oven where
evaluation is desired.   This is a coarse method of measurement;
however by direct  comparison with different ovens, some tentative
conclusions were made.   Some samples  made near oven 3-18 (high
pressure steam,  3/4" nozzle)  indicated an increase in coal carry-
over by a factor of  five to ten when compared to the results from
ovens using low  pressure steam.

   As a result  of these tests a pressure regulator was added to
the design of the  new  high pressure steam supply.  This would
permit regulating  the  pressure at a value less than 175 psi to
prevent excessive  coal carry-over.

   Further tests  were made to obtain more definitive results by
taking measurements  directly in the ascension pipes.  As a starting
point velocity and temperature of the ascension pipe gas were
measured.  The velocity of gas was determined from measurements
taken with a pitot tube and water manometer.  The pitot tube
transmits the static pressure to one side of the manometer, and
the dynamic pressure to the other side.   The velocity is then
proportional to  the  square root of the inches of water differential.
The annubar is a self  averaging pitot tube which eliminates the
need to traverse while taking measurements.  The results of the
two methods checked  within 15% giving confidence in the measurements,


                               284

-------
ASCENSION PIPE PARTICULATE SAMPLING  (continued)

    Tests were then made to sample the coal carry-over.  The
annubar measured the differential pressure so that the gas flow
rate could be calculated using the equation:
    Qn = 7.9 SNDy-^-  "h  (Refer to part A for details of equation)
    Coal samples were collected in an Alundum filter contained in
a sampling tube inserted in the ascension pipe.  A thermocouple
was used to measure the gas temperature.  The complete test
procedure is described in Part B.  Sample calculations are shown
in Part C.

    The quantitative evaluation of coal carry-over is subject to
error and the calculations represent an upper limiting value
that was probably never reached.  The material from which the ash
is derived represents various carbonaceous material from coal to
coke.  The ash content of coke and semi-coke materials is higher
than that of coal thus causing higher results.  Factors during
leveling such as the way in which the gas passageway is constricted
as well as the degree of port seals (particularly the leveler
door opening)  are expected to influence the amount of coal carry-
over.

    The results of this investigation indicated that the coal
carry-over during charging increased by a factor of about 6:1
for the high pressure steam.  This comparison was based on six
tests .

    A more accurate method of determining the amount of coal carry-
over involved taking tar samples from the #9 cross-over of P-4
battery with the aspirating steam header pressure at 130 psi
and then 180 psi.  These tar samples were collected in a 55 gallon
drum in such a manner that the excess flushing liquor was drained
off to the decanters.  The tar samples were taken just prior to
the point where the tar mixes with that of other batteries before
reaching the decanter.  The analysis of the tar from each sample
is shown in Table 6  (pg. 90a) .

    A microscopic analysis of the suspended solids was made by
repeatedly washing the tar with xylene.  'The filtered solids were
dried,  imbedded in an epoxy resin and polished.  Microscopic
examination of the polished specimens revealed that suspended
                               285

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ASCENSION PIPE  PARTICULATE SAMPLING  (continued)

solids consisted of very fine spherulitic carbon particles, coal,
semi-coke,  coke,  and pyrolytic carbon  (similar to wall  and roof
carbon), as shown in figure 77.  The spherulite carbon  is
derived  from the cracking or incomplete combustion of gases,
whereas  the coal and coke are derived  from the oven charge.   The
distribution of the carbon forms was determined and adjusted  to
the percent of  quinoline insolubles  in the tars.  These values,
shown in Table  28,  indicate that the tar collected at higher  steam
pressure had more and larger carbon  solids derived from coal  carbon-
ization.

    Based on a  value of 7 gallons of tar  (from flushing liquor)
and 16.7 tons of coal per charge, a  specific gravity of 1.20,
approximately 22.1 pounds of coal carry-over per charge occurs  at
130 psi  while the value at 180 psi was about 49 pounds  of coal.
This represents a lower limit, since some of the coal would
settle out  in the collecting main.
                                 286

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            PHOTOMICROGRAPHS - SUSPENDED SOLIDS IN TAR
                    300X
                      130 LBS.
                    300X
                      180 LBS.
600X
300X
PHOTOMICROGRAPHS SHOW SPHERULITIC CARBON (SC), COAL (C), COKE (CK)
OBTAINED FROM PITTSBURGH TAR COLLECTED WHILE P-4 BATTERY OPERATED
WITH INDICATED STEAM ASPIRATING PRESSURE.  BLACK AREAS ARE PORES AND
GRAY AREAS ARE PLASTIC IMBEDDING MATERIAL (PL). REFLECTED LIGHT.
                           FIGURE 77
                             286A

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Table 28.   DISTRIBUTION AND SIZE OF SUSPENDED SOLIDS IN TAR
                 (Varible steam pressure)
Wt.,%of Total Tar1
Steam Pressure, Ibs.
130 180
(Base) (Trial)
I
Spherulitic Carbon \ 6.1 4.8
\
Coal
Serai- coke
Coke
Pyrolytic Carbon
Quinoline Insolubles
in tar, (wt. ,%) ,
determined by
chemical analysis
(wt. %)
0.2 0.8
0.2 1.1
1.7 3.9
0.3 1.3
8.5 11.9
Header Steam Pressure, psi
130
Tyler
Microns Mesh

6 400
230 60-70
90 140-170
220 60-70
230 60-70

180
Tyler
Microns Mesh

6 400
430 35-40
350 40-45
430 35-40
460 35-40

 1.   Adjusted  to quinoline insoluble content
                           286b

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                              PART A

GAS FLOW EQUATION

    The equation used to determine gas velocity  from the differentia]
pressure measurements appears in the Annubar Technical Data/
Section C of the Ellison Instrument Division catalog under  the title
"Annubar Flow Calculation Report"

    Qn = 7.9 SND2  vrf
                    rl

    Since rf is related to rl this relation is reduced to:
    r,    -7 Q cMn   14.7 + PSIG of line    _ 520
    Qn = 7.9 SND   - — -  x
                                          _   _
                          — -    460 + line temp  (6F)


                                Fl

    The line pressure never exceeds a few inches of water,
consequently

    14.7 + PSIG of line     /^
         14.7
                    'v 460 + li
                              520
             2    v 460 + line temp (°F)   / -,
, Qn =  7.9  SND      	——	*—*	^ -J h n


 S= Constant factor for element at specific flow,
  = Kg Fv

 KG= geometrical  constant;  for element type 740 and 13"
    pipe,  Kg = 0.913

 Fv= velocity distribution  factor; for transition  and
    turbulent  flow,  Fv = 0.82

 S= Kg Fv = (0.913)(0.82)  = 0.75

 N= grouped constant including A/ 2g   (gravity acceleration,
     ""V4  (circular area) ,  and conversion constants which
    depend on  units chosen for Qn and ^n.

                             287

-------
GAS FLOW EQUATION (continued)

   Where Qn is expressed in CFM, and hn is expressed in inches
       of H20 corrected to 68°F.

   N=  0.7576

   D=  exact inside diameter of pipe (inches)

   rl= specific weight of gas at base conditions in pounds per
       cubic foot.   This is also equal to the specific gravity
       of gas at base conditions times the weight of air  (#/ft3)
       at base conditions.  Air = 0.0765 #/ft3 at standard  (60°F/
       14.73 psia)  base conditions.

       A value of 0.7 has been used for the specific gravity
       based on approximate results using Schillings apparatus.


   rf= specific weight at flowing conditions in pounds p.er cubic
       foot including compressibility.

       rf =  14.7 + PSIG line x 	520	 x r±
                  14.7          460 + line temp. (°F)

   For this application

   7.9 SND2 = 7.9 x 0.75 x 0.7576 x (13)2
            = 759

                                   520
   .Qn = 759                  W 460 + T line    A/ h
                                                   n
   Let rl = 0.7 x 0.0765 = 0.0535
         ^T = V"0-0535 = 0-231
                   /     520
       Qn = 3280 V 46o + T line X
                              288

-------
GAS FLOW EQUATION (continued)

    This equation can now be used to measure ascension pipe gas
flow (°-n) in CFM by determining the temperature of gas within
the ascension pipe and the differential pressure.  The effective
specific gravity of the gas must also be determined with reasonable
accuracy.
                               289

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                              PART B

 TEST  PROCEDURE

 Equipment  requirements  are as follows:

 1.  1 - Annubar

 2.  1 - Alundum  filter  holder and sampling tube

 3.  1 - Alundum  filter  for each test

 4.  1 - H2O filled manometer  36"

 5.  1 - Hg filled manometer 36"

 6.  1 - Thermometer  0°F to 250°F

 7.  1 - Thermocouple and wire

 8.  1 - Potentiometer

 9.  1 - Gas volume meter

10.  1 - Air aspirator

11.  Assorted stainless  steel  and  copper  tubing  with  fittings

12.  1-3" pipe  2' long threaded  one end.

 Procedure

    The tubing is cut to length and  assembled with fittings. One
 1" hole is drilled and  one 3"  hole  is drilled half way up  in each
 of the ascension pipes,  standpipes with the former hole being 3"
 above the latter hole.   A  1"  sleeve  and  a  3" sleeve  are welded to
 the standpipe to enable the holes to be  plugged and the
 instruments to be supported.

    The instruments  are assembled according to  Figures78,  and  79.

    The test is conducted  for  the first  60 to 70 seconds after
 the start of leveling.   The air aspirator  is turned  on as  soon*
 as leveling starts,   and  readings  are taken continuously by a four
                                290

-------
TEST PROCEDURE (continued

Procedure (continued)

man crew for 60 to 70 seconds.  One man each is required to read
the annubar's manometer; gas meter's manometer, thermometer and
gauges; the thermocouple's poteniometer; and to time with  a stop-
watch.  After the test,  the collected sample is taken to the
chemical lab where an analysis  is made of the collected particulate
to determine the amount of suspended solids.  This analysis consists
of weighing the particulate  (to determine the total weight),
rinsing with benzene and re-weighing (to determine the percentage
of tar), and burning the sample and weighing again  (to determine
the percentage of ash) .

    The data collected  during a test is used to calculate  the rate
of flow in SCFM and the amount  of coal carryover per standard
cubic  foot.  This data  are then used to calculate the ratio of coal
carryover with the high pressure steam versus coal carryover
with the low pressure steam.
                                291

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         TUBE fa
-  Tf-f.E.fZMOCOUF'^JS
TESTS OR S^MP&IMG;
                                                    /AT
TD. -
                                  78

-------
                -J/AJL.VZ.

          79
233

-------
                             PART C




SAMPLE CALCULATIONS




   Attached  are the data sheets from six tests made on  two


different  dates.  The calculated gas velocity  in the stand-

pipe  is determined with the following equation,
    Qn  =  3280
    *
                 Aein     -. .
                 460 + T line
    The  calculated volume of the metered gas sample is,



    Std.  Cubic  Feet = Vol. x /460_JL_68\      ( 30.
                             V460 + T  /      V.  30






    The  re-calculated sample weight is,





                              (% Coal  ash in sample
    Coal  Weight = sample wt. x/
                               % Coal ash in charged coal
                               i



    The  estimated coal carry-over per charge is,


                                   .   _    ,              Average
              -, / -L.        Grams coal ., Pounds    ._   ,„„  „ _,
    Pounds  coal/charge =  	3	 x 	 x  Qn  avg. x Charge
                             FtJ       Gram
                                                          Time
                               294

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Test  Data Summary  Sheet
Test No.
Date
Oven No.
Calculated Gas
Velocity
T line ' ^'
hn (" H20)
Qn (Eq. 1)
Calculated Metered
Gas Sample
Sample Vol. (Ft3)
Gas Temp, at gas
meter (°F)
Gas Pressure at
gas meter (" Hg)
Sample Vol. in
Std. cubic feet
Recalculated Sample
Weight
Sample Weight (g. )
% Coal Ash in Sample
% Coal Ash in Charged Coal
Recalculated Sample Wt. (g. )
Grams Coal Ft3 Gas
Pounds Coal Charging Cycle

1
9/6
3-24

2129
2. 3
2220 CFM
0. 5
90
-15 "
0. 24

3. 2
14. 3
7. 85
5.82
24.2
237
2
9/6
3-13

1453
0.676.
1410 CFM
. 45
118
-13. 4"
0. 228

1. 04
12.8
7. 85
1. 7
7.45
46. 3
3
9/13
3-18

1936
2. 1
2220 CFM
0. 3
110
-16"
0. 13

2.8
18.4
7. 84
6.58
50. 6
495
4
9/13
3-13

1993
0. 45
1020 CFM
0. 33
80
-15"
0. 161

2. 01
13.5
7.84
3.46
21.5
96
             295

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Test Data  Summary Sheet
Test No.
Date
Oven No.
Calculated Gas
Velocity
T line (°F)
hn ("H20)
Qn(Eq. i)
Calculated Meter ed
Gas Sample
Sample Vol. (Ft3)
Gas Temp, at gas
meter (°F)
Gas Pressure at
gas meter (" Hg)
Sample Vol. in
Std. cubic feet
Recalculated Sample
Weight
Sample Weight (g. )
% Coal Ash in Sample
% Coal Ash in Charged Coal
Recalculated Sample Wt. (g. )
Grams Coal Ft3 Gas
Pounds Coal Charging Cycle

5
9/13
3-24
1949
2.4
2360 CFM
. 21
78
-15
. 103

3.2
19.2
7.84
7.85
76.2
795
6
9/13
3-11
1895
. 4
975 CFM
.3
90
-15
. 144

.81
20. 3
7.84
2. 1
14.6
62.8
































              296

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       ASCENSION  PIPE  GAS SAMPLING DATA SHEET
                                                                 TEST 1
Date  September 6, 1971
Condition at Start  of Time
                                 Oven No.  3-24
                                                        Time   65 Seconds
                               Start of leveling
Reading


   2
   3
   4
   5
   6
                Time
               30 seconds
                     NOTE:
                                   Annubar
                                       (" H20)
                                                     Thermocouple    Calculated
                                     Z. 3
   Temp.  (°F)
     Z129°
Gas  Velocity
                                                                        2220 SCFM
                                     Other readings- during this test  were not
                                     properly recorded and were discarded.  This
                                     one valid reading appears to be representative
                                     of the average.
Gas Sample Meter Data
Measured Pressure (" Hg)
Measured Temperature (°F)
Metered Gas Sample (Ft3)
Timed Gas Sample  Period (Sec. )
Calculated Metered Gas (Std.  Cond. )
                                                       -15"
                                                      .90°
                                                       .5ft
                                                       65 sec.
                                                       . 24 SCF
Particulate Sample
Sample Weight
% Benzene Insol Fraction
                              3. 2 grams
                              98. 2%
Ash 14.3%
Recalculated Sample Weight    5, 82
    Calculated
                         Grams Coal
                         Ft3  Gas
                                       24.2
Sampling Condition
Coal Pulverization
Coal Moisture
Qts. Oil/Ton Coal
Header Steam Pressure
Ascension Pipe I. D.
                      Coal Ash
                                           7. 85%
                                          75.8% thru 1/8" screen
                                           6.5%
                                           3.55
                                           175 psi
                                            13'
                                     297

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       ASCENSION  PIPE GAS SAMPLING DATA SHEET
                                                               TEST 2
 Date   September 6,  1971
                   Oven No.     3-13     Time    67 seconds
 Condition at Start of Time	Start of leveling
 Reading

   1
   2
   3
   4
   5
   6
  Time
 0 second
12 seconds
24 seconds
36 seconds
48 seconds
60 seconds
 Gas Sample Meter Data
                       Average
Annubar
^P (" H20)

  .95"
 . . 90"
  .65"
  . 53"	
  .6"
  . 7"
  .676"
                                                     Thermocouple    Calculated
Measured Pressure (" Hg)
Measured Temperature (°F)
Metered Gas Sample (Ft3)
Timed Gas Sample Period (Sec. )
Calculated Metered Gas (Std.  Cond. )
Particulate Sample
Sample Weight
% Benzene Insol Fraction
                1. 04 grams
                99. 1%
Recalculated Sample Weight    i. 7
Temp.  (°F)

   1478
   1226
   1626
   1512
   1556
   1346
   1455
   -13.4"
   118°F
   .45 ft3
                                          67 sec
                                         . 228 ft3
              Ash 12.8%
Sampling Condition
Coal Pulverization
Coal Moisture
Qts. Oil/Ton Coal
Header Steam Pressure
Ascension Pipe I. D.
         Coal Ash
 7. 85%
                      75. K thru 1 /8"
                       6.5%
                       3.55
                        100 psi
                        13"
                                                       Gas  Velocity
                                                         1410 SCFM
Calculated
Grams Coal
Ft3 Gas
7,45 g/ft3
                                      298

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       ASCENSION  PIPE  GAS SAMPLING DATA SHEET
                                                               TEST 3
Date  September  13, 1971
                   Oven No.
                                            3-18
Condition at Start of Time    Start of leveling
                     Time    67 seconds
Reading

   1
   2
   3
   4
   5
   6
   Time
 0 second
Annubar
    " H2°)
20 seconds
40 seconds
60 seconds
 Average
                       2.2'
                       2.4'
 1.6'
                       2. I1
Gas Sample Meter Data
Measured Pressure (" Hg)
Measured Temperature (°F)
Metered Gas Sample (Ft3)
Timed Gas Sample  Period (Sec. )
Calculated Metered Gas (Std.  Cond. )
Particulate Sample
Sample Weight
% Benzene Insol Fraction
                2. 8 grams
                99.4
Recalculated Sample Weight
                  6.58
                                                     Thermocouple    Calculated
Temp. (°F)
                                          1690
                   2208
                    1827
                                          1772
                   1936
                                          -16
                                          1.10°
                                          .3 cu. ft.
                                          67 s.ec.
                                          . 130
              Ash    -18.4
Gas  Velocity
                   2220 SCFM
    Calculated
            Grams Coal
            Ft3  Gas
                                         50. 6
Sampling Condition
Coal Pulverization
Coal Moisture
Qts. Oil/Ton Coal
Header Steam Pressure
Ascension Pipe I. D.
         Coal Ash
                        7. 84%
                       74. 1% thru 1/8" screen
                        6. 60%	
                        3.03
                       175 psi
                        13'
                                     299

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       ASCENSION  PIPE! GAS SAMPLING DATA SHEET

                                            3-13
                                                                TEST 4
 Date  September  13, 1971
 Condition at Start of Time
                                Oven No.
                                                       Time   73 Seconds
                                    Start of leveling
                                   Annubar
 Reading

   1
   2
   3
   4
   5
   6
                Time
               0 second
                                                     Thermocouple   Calculated
             20 seconds
             40 seconds
             60 seconds
             73 seconds
               Average
                                     .6
                                     .6
.4
                                     .4
                                     .4
                                    .45
Gas Sample Meter Data
Measured Pressure (" Hg)
Measured Temperature (°F)
Metered Gas Sample (Ft3)
Timed  Gas Sample Period (Sec. )
Calculated Metered Gas (Std. Cond. )
                                                    Temp.  (°F)
                                                       972
                                                      1986
                  1995
                                                      1995
                                                      1995
                                                      1993
                                                       -15'
                                                      .80°
                                                      . 33	
                                                      73 sec.
                                                      . 161 SCF
Particulate Sample
Sample Weight
% Benzene Insol Fraction
                             2. 01 grams
                               3.3
          % Ash    13.5
Recalculated Sample Weight
                                 3.46
     Calculated
                         Grams Coal
                         Ft3  Gas
                                          21.5
Sampling Condition
Coal Pulverization
Coal Moisture
Qts. Oil/Ton Coal
Header Steam Pressure
Ascension Pipe I. D.
                      Coal Ash
 7.84%
                                    74. 1 % thru 1/8" screen
                                     6. 60%	
                                     3. 03'
                                    100 psi
                                     13"
                                Gas Velocity
                                                                       1020 SCFM
                                     300

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       ASCENSION  PIPE  GAS SAMPLING  DATA  SHEET
                                                                  TEST 5
Date    September 13, 1971
Condition at Start of Time
                  Oven No.
                                             3-24
                  Start of leveling
                     Time   67 Seconds
Reading

   1
   2
   3
   4
   5
   6
 Time
 0 second
Annubar,
    " H20)
                      3. 0
15 seconds
30 seconds
45 seconds
60 seconds
               Average
 2. 0
                      2. 5
                      Z.5
                      2.5
                                    2.4
Gas Sample Meter Data
Measured Pressure (" Hg)
Measured Temperature (°F)
Metered Gas Sample (Ft3)
Timed Gas Sample  Period (Sec. )
Calculated Metered Gas (Std.  Cond. )
Particulate Sample
Sample Weight
% Benzene Insol Fraction
                      3. 2 grams
                    99.2
Recalculated Sample Weight
                     7. 85 grams
                                                     Thermocouple    Calculated
Temp. (°F)
                                        1329
                                        1591
                                        2150
                                        2244
                   1811
                                                      1949
                                        -15	
                                         78	
                                        .21
                                         67	
                                         0. 103 .SCF
Gas  Velocity
              Ash
      19.2
    Calculated
           Grams Coal
           Ft3 Gas
        76.2
Sampling Condition
Coal Pulverization
Coal Moisture
Qts. Oil/Ton Coal
Header Steam Pressure
Ascension Pipe I. D.
        Coal Ash
                          7. I
                         74. 1% thru 1/8" screen
                          6. 60%	
                          3. 03
                          175 psi
                           13'
                                                          2360 SCFM
                                     301

-------
       ASCENSION  PIPE GAS SAMPLING DATA SHEET
                                                                  TEST 6
 Date  September 13,  1971
 Condition at Start of Time
                  Oven No.   3-11
                                         Time
                               67 Seconds
                                     Start of leveling
 Reading

    1
    2
    3
    4
    5
    6
 Time
 0 second
20 seconds
40 seconds
60 seconds
 Average
Annubar
    " H20)

  .6
  .4
  .4
  . 4	
  . 4
 Gas Sample Meter Data
 Measured Pressure (" Hg)
 Measured Temperature (°F)
 Metered Gas Sample (Ft3)
 Timed Gas Sample Period (Sec. )
 Calculated Metered  Gas (Std.  Cond. )
Particulate Sample
Sample Weight
% Benzene Insol Fraction
                81 grams
                99.4
Recalculated Sample Weight
                 2. 1 grams
                                                     Thermocouple    Calculated
     Calculated
          Grams Coal
          Ft3  Gas
                                     Temp. (°F)
                                        1329
                                        1957
                                        1772
                                        1957
1895
              Gas  Velocity
                                  Ash
                                     975 SCFM
                                        -15	
                                       _90	
                                        .3	
                                       _67	
                                        0. 144 SCF
                      20.3
         14. 6
Sampling Condition
Coal Pulverization
Coal Moisture
Qts. Oil/Ton Coal
Header Steam Pressure
Ascension Pipe I. D.
       Coal Ash
   7.84%
                      74.1% thru 1/8 screen
                       6.60%	
                       3. 03
                       100 psi
                         13'
                                     302

-------
                                 TECHNICAL REPORT DATA
                          (Please read liittructions on the reverse before completing)
 1 REPORT NO.
  EPA-650/2-74-022
                            2.
            3. RECIPIENT'S ACCESSION-NO.
 4. TITLE AND SUBTITLE
 Coke Charging Pollution Control Demonstration
                                                       5. REPORT DATE
                                                        March 1974
                                                       6. PERFORMING ORGANIZATION CODE
 7. AUTHOR(S)

 J.H. Stoltz
            8. PERFORMING ORGANIZATION REPORT NO.
 9. PERFORMING ORGANIZATION NAME AND ADDRESS
 Jones and Laughlin Steel Corp.
 Pittsburgh, Pa.  15219

 Contractor: American Iron and Steel Institute
            10. PROGRAM ELEMENT NO.
            1AB013; ROAP 21AFF-03
            11. CONTRACT/GRANT NO.
            CPA 70-162
 12. SPONSORING AGENCY NAME AND ADDRESS
 EPA, Office of Research and Development
 NERC-RTP, Control Systems Laboratory
 Research Triangle Park, N. C.  27711
            13. TYPE OF REPORT AMD PERIOD COVERED
            Final
            14. SPONSORING AGENCY CODE
 15. SUPPLEMENTARY NOTES
              report'gives results of demonstrating a coke oven charging system
 designed to reduce emissions sufficiently to both meet future air pollution control
 requirements and improve the environment on top of the battery for operating
 personnel. The work included detailed engineering,  construction, and testing of a
 prototype system on an existing battery with a single gas  collecting main.  The
 demonstration showed that, although emissions were reduced significantly, the system
 must be modified with a double gas off-take to satisfy air pollution control require-
 ments.  The system can be applied to new batteries or to  existing batteries where a
 double gas off-take exists or  can be obtained by such means  as a second collecting
 main or jumper pipes.  The battery top environment was improved for the larry car
 operator by having the charging sequence performed from within an air-conditioned
 cab. Although a lidman is required on the top side of the battery,  his work conditions
 were improved by having the  larry car perform lidding and dampering operations.
17.
                              KEY WORDS AND DOCUMENT ANALYSIS
                 DESCRIPTORS
                                           b.IDENTIFIERS/OPEN ENDED TERMS
                         c. COSATt Field/Group
 Air Pollution            Leveling
 Iron and Steel Industry  Ovens
 Coking                  Pressure
 Metallurgical  Fuels       Control
 Automation
 Feeders
Air Pollution Control
Stationary Sources
Coal Charging
Charging on Main
Controlled Feed
13B
11F
13H
21D
13A
 3. DISTRIBUTION STATEMENT


       Unlimited
19. SECURITY CLASS (This Report)
  Unclassified	
                                                                    21. NO. OF PAGES
   325
20. SECURITY CLASS (Thispage)
   Unclassified
                         22. PRICE
EPA Form 2220-1 (9-73)
                                    304

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