Environmental Protection Technology Series
ALUM  ADDITION  AND STEP-FEED STUDIES
             IN  OXYGEN-ACTIVATED SLUDGE
                       Municipal Environmental Research Laboratory
                            Office of Research and Development
                            U.S. Environmental Protection Agency
                                    Cincinnati, Ohio 45268

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                RESEARCH REPORTING SERIES

Research reports of the Office of Research and Development, U.S. Environmental
Protection Agency, have been grouped into nine series. These nine broad cate-
gories were established to facilitate further development and application of en-
vironmental technology. Elimination of traditional grouping was consciously
planned to foster technology transfer and a maximum interface in related fields.
The nine series are:

      1.  Environmental Health Effects Research
      2.  Environmental Protection Technology
      3.  Ecological Research
      4.  Environmental Monitoring
      5.  Socioeconomic Environmental Studies
      6.  Scientific and Technical Assessment Reports (STAR)
      7.  Interagency Energy-Environment Research and Development
      8.  "Special" Reports
      9.  Miscellaneous Reports

This report has been assigned to the ENVIRONMENTAL PROTECTION TECH-
NOLOGY series. This series describes research performed to develop and dem-
onstrate instrumentation, equipment, and methodology to repair or prevent en-
vironmental degradation from point and non-point sources of pollution. This work
provides the new or improved technology required for the control and treatment
of pollution sources to meet environmental quality standards.
This document is available to the public through the National Technical Informa-
tion Service, Springfield, Virginia 22161.

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                                                 EPA-600/2-77-166
                                                 September  1977
         ALUM ADDITION AND STEP-FEED STUDIES
                         IN
               OXYGEN-ACTIVATED SLUDGE
                         by

Dolloff F. Bishop, James A. Heidman,  Richard C.  Brenner
                         and
                  John B. Stamberg
                 EPA-DC Pilot Plant
               Washington, D.C.  20032
               Contract No. 68-01-0162
                   Project Officer

                  Dolloff F. Bishop
            Wastewater Research Division
     Municipal Environmental Research Laboratory
               Cincinnati, Ohio  45268
       This study was conducted in cooperation
                        with
     the Government of the District of Columbia
        Department of Environmental Services
               Washington, D.C.  20004
     MUNICIPAL ENVIRONMENTAL RESEARCH LABORATORY
         OFFICE OF RESEARCH AND DEVELOPMENT
        U.S. ENVIRONMENTAL PROTECTION AGENCY
               CINCINNATI, OHIO  45268

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                                DISCLAIMER
This report has been reviewed by the Municipal Environmental  Research
Laboratory, U.S. Environmental Protection Agency,  and  approved  for publication.
Approval does not signify that the contents necessarily  reflect the views and
policies of the U.S. Environmental Protection Agency,  nor does  mention of trade
names or commercial products constitute endorsement  or recommendation for use.
                                      11

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                                  FOREWORD
The Environmental Protection Agency was created because of  increasing public
and government concern about the dangers of pollution to the health and
welfare of the American people.  Noxious air,  foul water, and spoiled land
are tragic testimony to the deterioration of our natural environment. The
complexity of that environment and the interplay between its components
require a concentrated and integrated attack on the problem.

Research and development is that necessary first step in problem solution and
it involves defining the problem, measuring its impact, and searching for
solutions.  The Municipal Environmental Research Laboratory develops new and
improved technology and systems for the prevention, treatment,  and  management
of wastewater and solid and hazardous waste pollutant discharges from muni-
cipal and community sources, for the preservation and treatment of  public
drinking water supplies, and to minimize the adverse economic,  social, health,
and aesthetic effects of pollution.  This publication is one of the products
of that research; a most vital communications link between  the  researcher and
the user community.

The use of pure oxygen in the activated sludge process for  removal  of organic
pollutants from wastewater and thus from the aqueous environment is being
employed in an increasing number of treatment plants.  This work describes
firstly the use of mineral (alum) addition within the oxygen-activated sludge
process to increase the removal of the phosphorus nutrients from the waste-
water and secondly, an alternate process configuration for  contacting the
oxygen and the wastewater.
                              Francis T. Mayo
                              Director
                              Municipal Environmental Research Laboratory
                                     iii

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                                   ABSTRACT

 A plug flow, (^-activated sludge process was operated  with alum  addition  to
 remove phosphorus and with lime addition to prevent  the  process  pH from
 decreasing below 6.4.  The G£ reactor was operated at  F/M  ratios between
 0.18 to 0.24 gm of BOD5/gm of MLVSS/day with the  SRT varying  from 4.7  to  6.0
 days in a typical co-current C^-liquid contacting system.

 The average alum (Al2(804)3  ' -^ H2°) dosages for the  five steady-state
 operating periods increased  from 84 mg/1 to 184 mg/1 with  the M/P weight
 ratios increasing from 1.1 to 2.66.   The amount of lime  required  to maintain
 the process pH at 6.4 or  above varied from 15 mg/1 to  58 mg/1 as  CaO.  The
 lime demand was related to both the alum addition and  to partial  nitrification
 occurring in the oxygen reactor.

 The pollutant removals from  the primary effluent  ranged  from  82  to 92% for
 BOD5 (7.4 to 19 mg/1  of residual  BOD5),  from 52 to 84% for suspended solids
 (17 to 56 mg/1 of residual SS),  and from 54 to 86% for phosphorus (1.05 to
3.26 ™g/l of residual P).  The  optimum P removal  occurred  at  a 1.8 to 1
 average Al/P ratio with an average total residual P  of 1.05 mg/1.

 In  a second study,  the 02  process was operated in a  step-feed configuration
 consisting of  a sludge oxygenation stage followed by three  stages of oxygen
 aeration  with equal portions  of  the primary effluent fed to each  stage.  In
 typical operation,  the process  with a F/M  ratio of 0.23  exhibited a MLSS
 concentration  profile in the  four stages of  10,700 mg/1; 7,060 mg/1; 5,020
mg/1;  and  4,150 mg/1.   The step configuration  clearly reduced the solids
 loading to the  clarifier and  provided  an average  process MLSS of more than
 6,500 mg/1.

The  step operation produced excellent  BOD^  removals  (89% from the primary
effluent)  with  an effluent BOD5 of 10 mg/1  and a  soluble (filtered) effluent
BOD5 of less than 3 mg/1.   The COD and  suspended  solids residual  averaged
43 mg/1 and  23 mg/1, respectively.

Oxygen balances, based upon inlet and outlet 02 measurements and alternately
upon 02 uptake rates and upon the amount of 02 in the outlet gas, revealed
an 02 usage of approximately 50%.  The 02 usage in the step configuration was
significantly less than the 90% typically achieved in co-current contacting.

This report was submitted in partial fulfillment of Contract No.  68-01-0162 by
the government of the District of Columbia, Department of Environmental Services
under the  sponsorship of the U.S. Environmental Protection Agency.  This report
covers experimental work conducted during the period  October  1972-October 1973.

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                              CONTENTS

Foreword	iii
Abstract	,  . iv
List of Figures	vi
List of Tables	vii
Acknowledgements	viii
     1.  Introduction  	  4
     2.  Conclusions 	  1
     3.  Recommendations	3
     4.  Pilot System  	  6
     5.  Analytical Procedures 	  8
     6.  Alum Addition Studies 	  9
     7.  Step-Feed Studies 	 21
References	30
Publications 	 31
                                v

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                                 FIGURES


Number                                                              Page

  1   Oxygen Aeration System 	   7

  2   Phosphorus Removal by Alum Addition in
        (^-Activated Sludge	14

  3   Initial Settling Velocities of  Oxygen MLSS as  a
        Function of Concentration  	  16

  4   Typical Step-02 MLSS Settling  	  23

  5   D.O.  Uptake as a Function  of  Time-Stage No.  1  and  2   	  27

  6   D.O.  Uptake as a Function  of  Time-Stage No.  3  and  4	28
                                 vi

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                                    TABLES

Number                                                                      Page

  1   Reactor Operating Conditions for (^-Activated Sludge
        with Alum	10

  2   Clarifier Operation and Sludge Production of 02~Activated
        Sludge with Alum Addition	11

  3   Effluent Quality of 02~Activated Sludge with Alum Addition  	  13

  4   Settling Rates for 02-Activated Sludge with Alum Addition	15

  5   Filtration System on Alum-Qr, Secondary Effluent	18

  6   Filter Performance on Alum-0« Secondary Effluent  	  19

  7   Step-Feed, 02~Activated Sludge Operating Conditions 	  22

  8   Initial Settling Velocities of Step-Feed,
        02-Activated Sludge 	  24

  9   Step-Feed, 02-Activated Sludge Effluent Quality 	  25
                                      vii

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                              ACKNOWLEDGEMENTS

The assistance of the operators,  technicians and laboratory staff  at the
EPA-DC Pilot Plant is gratefully acknowledged.
                                 viii

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                                 SECTION 1

                                INTRODUCTION

The oxygen-activated sludge process with more than 90% utilization of oxygen
has developed in recent years into a significant competitor with conventional
aeration for removal of BOD,- from xvastewater.  The process has been studied
since 1970 at the EPA-DC Pilot Plant1'2 in Washington, D.C.; the study has
revealed several advantages over conventional aeration.

The high oxygen transfer rates with pure Q^ produce high dissolved oxygen (D.O.)
concentrations and permit the use of high mixed liquor concentrations and thus
small reactors.  The high D.O. in the reactor minimizes periods of lowD.O.,
such as occur in clarification, and increases Oo transfer into the center of
the sludge mass.  The process exhibits apparently higher metabolic rates and
good resistance to shock organic loadings.  The high oxygen transfer rates
provide process flexibility for minimizing sludge production through easily
increased endogenous respiration in the reactor.

In evaluating oxygen applications, the process stability and reduced reactor
size must be weighed against the cost of the oxygen and the mechanical systems
employed in its utilization.  In addition, the increased mixed liquor concen-
trations possible in the oxygen process increases the mass loading on the
clarifier, which increases clarifier size.  Finally, sludge reduction through
increased endogenous respiration requires a stoichiometric amount of 02 for
each unit amount of COD destroyed.  The final design of the oxygen process and
its solids-handling system requires the consideration and balancing of these
factors with the ultimate cost benefit to be fully determined in the market
place over the next few years.

With the current usage of the 02~activated sludge process, consideration of
its compatibility with other wastewater treatment processes and development of
techniques to reduce mass loading on the oxygen clarifier are needed.  In pre-
vious work, alum addition1 to remove phosphorus (Equation 1) was applied to
the Q£ process on a wastewater of moderate alkalinity  (130 mg/1 as CaCO-j).
With the recirculation of 0^ within each reactor stage, the CO™, increasing in
recirculated process gas, normally suppressed the Washington, B.C. effluent pH
to a range of 6.4 to 6.6 without alum addition.  In the study with alum addi-
tion, the Al/P weight ratio was incrementally increased from 1.1:1 to 1.85:1
during a period of approximately one month.  At an Al/P weight ratio of 1.85:1,
the acid produced (Equation 2) by the hydrolysis of excess Al    further
reduced the 02 process wastewater pH from its normal 6.4 to 6.6 range to less
than 6.0.
          Al    + P04   ->  A1P04                   (1)
                  3HOH  -»  A1(OH)3 + 3H+           (2)

                                       1

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At the low pH, the process immediately removed more than 90% of the P
but within three days exhibited a dispersion of the biological and chemical
solids into the final effluent.  At a 1.4:1 Al/P ratio, the process waste-
water pH and alkalinity decreased only slightly and the bio-mass dispersion
did not occur but the alum addition removed only 80% of the P.  During the
alum addition, the chemical precipitates increased the amount of solids in
the reactor and the solids loading to the final clarifier.

Therefore, two studies on the activated sludge process were
performed at the EPA-DC Pilot Plant:  one, to further evaluate alum addition
for phosphorus removal using lime for pH control; the other, to evaluate a
step-feed configuration without mineral addition to reduce  the solids loading
to the final clarifier.

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                                  SECTION 2

                                 CONCLUSIONS
ALUM ADDITION  STUDIES

In earlier work  with alum addition in the oxygen-activated sludge process on
D.C. wastewater, increasing the Al/P dosage weight ratio to 1.85:1 depressed
the process pH from approximately 6.4 to below pH 6.  Within three days, the
process exhibited a dispersion of both chemical and biological solids into
the process effluent.  In the current study on alum addition for phosphorus
removal, lime  slurry added to the influent wastewater maintained the effluent
pH above 6.4 and prevented sudden dispersion of the biological and chemical
solids in the  clarifier.

The alum addition in the oxygen-activated sludge process, evaluated at four
average levels of Al/P dosage weight ratios (1.1:1, 1.45:1, 1.8:1, and 2.66:1),
produced a maximum phosphorus removal of 86% at the 1.81 Al/P weight ratio.

At the 1.8:1 Al/P weight ratio, the process exhibited maximum removals of
BOD5 (92%) and suspended solids (84%), with an average BOD5 residual of 7.4
mg/1 and a suspended solids residual of 17 mg/1.

At an average  Al/P weight ratio of 2.66, the process exhibited a gradual in-
crease of nonbiological solids in the process effluent.  The excessive amounts
of Al (OH)-} accumulated during 14 days of operation gradually increased
clarifier instability and forced discontinuance of the alum feed.

The average lime dose required to maintain the process pH of 6.4 was 15 and
37 mg/1 at respective Al/P weight ratios of 1.8 and 2.66:1.  Based upon a 1:1
molar Al/P requirement for precipitation of the phosphorus, these lime dosages
corresponded approximately stoichiometrically to the milli-equivalents of acid
produced by the hydrolysis of excess Al"1"^" ions to A1(OH)_.

Lime dosages above the stoichiometric requirements for hydrolysis of excess
Al"*""*"^ ions were also required to neutralize the HNO^ produced when the process
was partially nitrifying.

Solids production of 02~activated sludge with alum addition increased over
that for operation of the biological process without mineral addition.  During
operation with Al/P weight ratios ranging from 1.1:1 to 2.66:1 and for an
overall Al/P weight ratio of 1.53:1, the solids production averaged approxi-
mately 1.34 gm of solids per gm of applied BODtj, of which 0.99 gm of solids
per gm of applied BODr was in the wasted sludge.

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 STEP-FEED STUDIES

 The 02~activated  sludge  process operated  in a  step-feed configuration, as when
 operated  in the conventional  "plug"  flow  configuration, removed essentially
 all soluble substrate, with the soluble effluent BOD 5 averaging less than
 3 mg/1.

 The step-feed  configuration exhibited a MLSS profile that decreased from
 nearly 10,000  mg/1  in the first stage to  about 4,000 mg/1 in the fourth stage
 and averaged 6,500 mg/1.  The  4,000 mg/1 MLSS  in the fourth stage produced a
 desirable and  modest solids loading  [clarifier flux of about 115 kg/d/m
 (23 Ib/d/ft )].   Thus, the  step-feed configuration permitted a high average
 MLSS without a high flux loading to  the clarifier.

 The step-feed  configuration for  the 0? process, however, achieved only a 50%
 utilization of the C>2 gas feed  compared to the typical 90% utilization for
 the "plug"  flow configuration.   If further work confirms the 50% G£ utilization
 efficiency, the step-feed configuration will not be an economical alternative
 in  the 0?-activated sludge  process as practiced at the EPA-DC Pilot Plant.

 The  solids  production in  the  step-feed configuration at an SRT of approxi-
mately 11 days was 0.5 gm of solids produced per gm of applied BOD-, with
 approximately half of the solids production leaving the process in the
 secondary effluent.

The Deactivated  sludge process in the step-feed configuration produced
approximately 70% nitrification of the TKN at an SRT of 11 days and removed
approximately 40% of the total nitrogen.

The settling velocities of oxygen-activated sludge mixed liquor in the step-
feed configuration were good.   At a MLSS of approximately 4,000 mg/1,  the
solids exhibited initial settling velocities of 5.2 m/hr (17 ft/hr) which was
typical of summer  time  settling of 0~-activated sludge solids.

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                                 SECTION  3

                               RECOMMENDATIONS
ALUM ADDITION STUDIES

In the study, the oxygen-activated sludge system functioned satisfactorily at
an average alum dosage  (Period 3) which corresponded to an Al/P weight ratio
of 1.8.  Increasing the average alum dosage to correspond to an Al/P  weight
ratio of 2.66 (Period 4), even with pH control, produced a gradual process
failure.  In addition, without continuous phosphorus analyses on the primary
wastewater, the control of the daily and instantaneous Al/P ratio was not
very good.  Thus, the process behavior and the lower limit of the effluent
residual P concentration needs further study in a system with effective
instantaneous Al/P dosage control at Al/P  weight ratios  between  1.8 and  2.66.

STEP-FEED STUDIES

While the step-feed configuration on the oxygen-activated sludge process
reduced the mass loading to the final clarifier and also achieved efficient
BOD,- removal, the observed poor oxygen utilization efficiency would prevent
in the step-feed configuration practical applications of the oxygen contacting
system employed in the EPA-DC Pilot Plant.  Confirmation of the observed
oxygen utilization efficiency is needed.  Work on alternate oxygen contacting
approaches should also be performed to determine if practical (reasonable
oxygen utilization) operations can be achieved for an oxygen step-feed acti-
vated sludge configuration.

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                                   SECTION 4

                                 PILOT SYSTEM
 In the EPA-DC Pilot Plant, the oxygen-activated sludge equipment (Figure 1)
 consisted of a four-stage reactor of 30.5 nr* (8,080 gallon)  liquid  volume,
 and two center-feed gravity settlers with 7.25 m^ (78 ft^)  of clarification
 area in each settler and water sidewall depth of 3.4 m (11.1 ft.).   The gas-
 tight reactor included submerged hydraulic entrances and  exits with water
 seals where the mixing equipment enters the reactor.

 The reactor was divided into four mixing stages.   Oxygen  was introduced into
 the first stage; its flow controlled by a pressure regulator to maintain a
 pre-selected reactor gas pressure, usually between 2.54 cm  (1 inch)  and
 9.16 cm (4 inches)  of water.   The oxygen flowed from the  first through  the
 fourth stage and for normal "plug" flow operation was co-current to  the mixed
 liquor flow.  Compressors on each stage recirculated the  overhead gas through
 a  rotating diffusion-impeller to provide mixing of the bio-mass and  to  disperse
 the recirculating gas.   Variations in the compressor recirculation  rate,
 selected  manually by the operator, were used to control the  dissolved oxygen
 level  for plug  flow between 4 and 8 mg/1.

 In the center-feed  settlers,  two sludge withdrawal mechanisms were employed:
 one settler  mechanism employed a hydraulic syphon;  the other,  a. conventional
 plow to force  the sludge into a  central sludge  well.   Sludge  recirculation
 was achieved by variable-speed Moyno sludge  pumps.

 In the  study of  mineral  addition,  the  reactor was  operated with various
 diurnal flow patterns in a  "plug" flow configuration with District of Columbia
 primary effluent as  the  process  feed.   Lime  slurry was added  to  the wastewater
 at the reactor  influent  and alum  was added at the  reactor discharge.  The lime
 slurry dosage was controlled  in  a flow-proportioned  (feedforward), pH error
 (feedback) analog control loop by a submerged pH probe located  in the first
 reactor stage.   The  pH set point  was manually altered  by the operator to main-
 tain the final process effluent pH in  the  range of 6.3  to 6.8.  The manually-
 selected alum dosage was proportioned  to flow by using  a pneumatically
 controlled metering  pump.

 In the step-feed study, the District of Columbia primary effluent was divided
 by a splitter box into three separate equal  streams  and pumped at a steady
flow into the last three stages of  the reactor.  Alum was not added to the
process.  In the step-feed study,  the 02 reactor employed the normal contacting
procedures and gas flow configuration.

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    02
           O2 RECYLE
•1
 l

 i
INFLUENT
                  db
                     ob
cb
                 SLUDGE RECYCLE
                                          ••-EXHAUST GAS
                                           JT
                                            I L
                                                    EFFLUENT
                                                     WASTE
    Figure 1. Oxygen aeration system.

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                                SECTION 5

                           ANALYTICAL PROCEDURES

 In the  evaluation of  the process  performance,  BOD  samples were always
 manually composited proportional  to  flow over  a  24-hour period.  All other
 appropriate samples were composited  for 24-hour  periods on Tuesday  through
 Thursday and for  48-hour periods  on  Friday  through Monday.  All  samples
 were  stored at  3°C to minimize  biological activity.  All samples except
 for BOD and suspended solids were also acidified with  1 ml of t^SO^ per
 600 ml  of sample.

 The 5-day biological  oxygen demand (6005) of the composite samples was de-
 termined by means of  the probe  method^;  the ammonia^ and nitrate-nitrite^
 by use  of  a Technicon Automatic Analyzer.  The total organic carbon (TOC)
 was measured on a Beckman Carbonaceous Analyzer.   The  total phosphorus" was
 determined by means of the persulfate  method.  All other analyses employed
 Standard Methods^.  Soluble phosphorus and soluble BOD were filtered through
 a  standard-glass  suspended-solids  filter  before  analyses.

 Batch settling  tests  on the process  mixed liquor were periodically conducted
 in a stirred 15.3  cm  (6-inch) diameter by 3.3 m  (10 feet) long "plexiglas"
 settling  column.   The slope of  the interface height versus time  provided
 the initial  settling  velocity of  the mixed-liquor  suspended-solids con-
 centration at the  existing wastewater  temperature.

 Dissolved  oxygen  uptake rates on  samples  of the  mixed liquor from various
 reactor stages  were conducted as appropriate.  In  the test, the mixed
 liquor sample,  usually with 4 to 8 mg/1 of D.O., was placed in a
 standard BOD bottle;   and  the dissolved  oxygen concentration was  continuously
measured with a D.O.  meter as a function of time.  The oxygen uptake rate
was then calculated as  the slope of  the D.O. versus time plotted for the
mixed liquor solids concentration  in the sample.

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                                  SECTION 6

                            ALUM ADDITION STUDIES
The operation of the process during alum addition studies was divided into
five operating periods  (Table 1) and a two-week period in February (period 4a
and 4b) for correcting  an accumulation of excess solids in the clarifier.  The
combination of reactor  contact time and average MLVSS provided relatively
constant F/M  (0.18 to 0.24 gm of BOD5/gm of MLVSS/day) and SRT (4.7 to 6.0
days) operation during  the five operating periods.   The diurnal flows (Table 2)
were usually varied for an approximate 1.5:1 peak to average flow ratio,
although in November the variation was 2:1 and in December 1.2:1.  During the
study, the influent pH  averaged 7; the effluent pH was maintained at or above
pH 6.4 with the addition of lime slurry.

During the first four periods, the average alum dose was increased from a 1.1
to a 2.66 Al/P weight ratio.  During the last period (March 1-20), the Al/P
weight ratio was averaged at 1.78.  Surprisingly, the lime dosage (Table 1)
decreased with increasing alum dosages in the first four periods.  Actually, in
the first period (November) with little excess Al    ions, HN03 production by
nitrification within the 02 process produced part of the lime demand.  In
December, a combination of partial nitrification, an elevated effluent pH of
6.7 with corresponding C02 neutralization (the normal operating pH is approxi-
mately 6.4 for Oo-activated sludge in Washington, D.C.), and the hydrolysis
of the excess Al    ions (Equation 2) all contributed to the 58 mg/1 CaO dosage.
In January, the elevated pH of 6.6 and the hydrolysis of the excess Al    ions
determined the lime requirement.

In the last two periods (February 1-14 and March 1-20) with the effluent pH at
6.4 and without nitrification, the lime dosages (15 ing/1 of CaO at a 1.78 Al/P
ratio and 37 mg/1 at a  2.66 Al/P ratio) corresponded almost stoichiometrically
to the amount of acid produced by the hydrolysis of the excess Al    ions
(Equation 2).   Clearly, only modest lime doses were required to prevent pH
depression caused by the addition of excess mineral salts for efficient phos-
phorus removal in the Q£ process.  It should be emphasized, however, that the
combination of partial nitrification and elevated effluent pH (above that
normally produced without mineral addition by CO,., adsorption in the process
wastewater) significantly increased the lime dosage.

During the entire study, the sludge production (Table 2) averaged 1.34 gm of
solids/gm of BOD,- applied.  The average operating conditions corresponding to
the sludge production was an influent BOD^ of 101 mg/1, an Al/P of 1.53, and
an alum dose of 115 mg/1.  In January, the decreased concentration of sludge
at the bottom of the clarifiers and the increased capture of solids produced an

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                     TABLE 1.   REACTOR OPERATING CONDITIONS FOR DEACTIVATED SLUDGE WITH ALUM
Period
Date
Reactor Detention hrs
F/M gra BOD5
(gm MLVSS) (day)
SRT days
MLSS
mg/1
% Vol.
CaO Dose
mg/1
PH
^ In
0 Out
Alkalinity as
CaC03, mg/1
In
Out
Alum Dose , mg/1
Al/P Weight Ratiob
(N03 4- N02) - N,
mg/1 in Eff.
1
Nov '72
2.6

0.21
5.8

6915
65

50.7

7.0
6.4


127
99
84
1.1

7.28
2
Dec '72
2.5

0.22
5,5

6840
61.3

58.0

7.0
6.7


116
134
105
1.45

3.53
3
Jan '73
2.76

0,20
6.0

6760
61

38.7

7.0
6.6


130
136
142
1.82

0.46
4
Feb 1-14
2.95

0.18
5.4

7060
58.5

37.4

7.0
6.4


114
101
184
2.66

0.25
4a
Feb 15-22C
3.43

0.16
3.5

6950
62.5

20

7.0
6.7


121
152
	


0.14
4b
Feb 23-28d
3.0

0.28
4.5

5380
66

15

7.0
6.5


130
126
105
1.1


5
Mar 1-20
3.0

0.24
4.7

5375
65.6

15.1

7.0
.6.4


129
116
136
1.78

0.15
aAlum as Al-CSO,)-  '  14H Q average daily dosage 115 mg/1.
DAverage daily Al/P £01? November^March 1.53..
'Alum addition discontinued;  heavy wasting applied  to remove  accumulated  chemical  solids.
 Alum addition resumed  at a 1..1 Al/P weight ratio;  darifier  bed  level  reestablished at
   usual 5-6 ft.  depth.

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     TABLE 2.   CLARIFIER OPERATION AND SLUDGE  PRODUCTION OF 0  ACTIVATED SLUDGE WITH ALUM ADDITION
Period
1
z..
3
4
4a
4b
5
Date
Nov. 1972
Dec. 1972
Jan. 1973
Feb. 1-14
Feb. 15-22
Feb. 23-28
Mar. 1-20
Average
Clarifier
Overflow
(m/d)
19.2
19.9
18.3
17.1
14.7
16.7
16.8
Peak to
Average
Flow
2
1.2
1.45
1.6
1.0
1.6
1.55
SVI
(nnl/g)
44
41
47
48
58
56
58
Recycle
Rate (%}
43
47
52
52
47
46
50
Underflow Solids (%)
Plow
2.39
2.15
2.04
2.0
2.43
1.57
1.63
Tow-Bro
2.19
2.14
2.04
2.04
2.34
1.76
1.83
Solids Production
(gm solids/gm BOD applied)
Produced3-
1 . 24
1.33
0.91
1.68C
2.83°
1.30°
1.34
Wastedb
.93
1.05
0.73
1.34
1.88
.88
.82
a The average sludge production for the study was 1.34 gm/gm of applied BOD5.   The  average  operating
  characteristics corresponding to the sludge production were an applied BODs  of 101  mg/1,  an Al/P of 1.53,
  and an alum dose of L15 mg/1.
  The average sludge wasted for the study was 0.99 gm/gm of applied
under conditions  as  in  note  1.
  The average sludge production for Feb. 1-28 was 1.92 gm/gm applied BOD .

-------
 increasing inventory of solids in the clarifiers.   Although' increased  wasting
 rates were employed in early February, the high alum dosage for February 1-14
 further increased the total solids inventory and the height of  the sludge
 blanket in the clarifiers.  Increasing amounts of  solids,  chiefly chemical
 solids, appeared in the clarifiers' overflow.  To  eliminate the increased
 solids inventory and the excessive carryover of solids in  the effluent,  the
 alum addition was discontinued for eight days in February  (15-22) and  heavy
 wasting was applied to the process.  Thus, while solids production during the
 first two periods (November and December) and last period  (March 1-20) repre-
 sented production at approximate equilibrium conditions, the sludge production
 in January was lower and in February was higher than expected production at
 equilibrium conditions.

 The BOD,  COD, SS, and  P  removals (Table 3) generally increased  with Al/P dosage
 ratios until the 2,66  Al/P ratio was applied.   The best removals occurred at
 the 1.8 Al/P ratio.  As  indicated earlier, at the  2.66 Al/P ratio the  process
 exhibited a gradually  increasing carry-over of chiefly chemical solids.   The
 accumulated solids from  January and the high Al/P  dosage caused increased
 sludge blanket depth within the clarifier and contributed  to the deterioration
 in effluent quality.   The  average pH was maintained at 6.4 and  the increased
 solids carry-over did  not  result from low pH.   The solids  in the process did
 not disperse suddenly; but even with an increased  wasting  of sludge, the con-
 tinued addition of a large excess alum caused  further  deterioration.   The alum
 feed was  discontinued  on February 15 and high wasting  rates were applied to the
 process to eliminate the excess sludge.   After eight days  of  operation,  the
 sludge blanket level was restored to the normal operating  level and  alum dosing
 was resumed,  but  at  a  1.1  Al/P ratio.   During  the  heavy wasting,  heavy solids
 carry-over occurred  in the clarifier.   Although the BOD  removal declined only
 moderately (from  about 90% to  81%),  COD,  SS,  and phosphorus removals declined
 markedly.   Thus, many of the materials in the  effluent were biologically
 difficult  to  degrade or  were chemical  solids.

 With the resumption of alum addition,  the process  exhibited  satisfactory BOD
 removals of about  85%, but high solids,  COD, and P  continued  to appear in the
 effluent for  the remainder of  the study.   Clearly,  the last  period  (March 1-20)
 of  the  study  did not represent  typical product  quality for mineral addition
 in  the 02  process.

 The  process influent and effluent  exhibited a wide  daily variation in phos-
 phorus content during the  operation from  November  through January.   Since the
 alum dosage was proportioned to flow,  the daily variation  in phosphorus  content,
 with some drift in the alum metering pump, produced the  range of Al/P shown in
Figure 2.   This figure clearly revealed not only the decrease in P with  in-
 creasing Al/P dosage ratio, but also a wide variation  in daily  P removal.  With
 the combined  sewers in the District of Columbia causing  the wide daily variation
 in influent P, we decided  that  improved Al/P dosage control would be useful.
During the study, fully automatic control, however, was not employed because  it
required the development of a continuous  analyzer for  influent P.
                                       12

-------
                       3.  EFFLUENT QUALITY OF 02 ACTIVATED SLUDGE WITH ALUM ADDITION3
BOD(mg/l)
'c-rlod Al/P
1 1.1
2 1 . 45
3 1.82
4 2.66
4,,
4b 1.1
5 1.78
In
104
100
97
91
100
91
108
Out
19.1
9.5
7.4
10.2
19.3
12.7
16
% Rem.
82
90
92
89
81
86
85
COD(mg/l)
In
238
241
246
220
247
249
246
Out
48
49
39
45
103
82
76
% Rem.
80
80
84
80
58
63
69
In
112
116
110
104
110
104
117
SS(mg/l)
Out
33
30
17
31
96
49
56
% Rom.
70
74
84
70
13
53
52
P(mg/l)
In
6.98
6.75
7.24
6.45
7.22
8.55
7.12
Out
1.84
1.72
1.05
1.32
4.64
4.05
3.26
% Rem.
74
75
86
79
36
53
54
N(mg/l)
In
23.8
26.9
25.9
23.2
22.8
23.5
25.0
Out
12.7
13.3
18.8
18.0
20.9
19.5
19.6
•\ Re,
48
36
28
22
8
17
'V ' '
aPercentage removals has eld upon primary effluent.

-------
    10
     8
  Q.

  CO  6
  O)
  CO

  I4

  Q_
  CO
  03
  0.
     1-
                         o
           00°
            o
                   o INFLUENT
                   • EFFLUENT

                6.2—6.8pH range

                   11/72-1/73
 o
o
                      °  oo
                         8
o
  °  oo
89)
   o
               o o
                  o
      o  CD  °° ° oo
     o o     00°
        o     o
             o   o
                o
            o   o
            o

             o
                                                 o
                                                 o
                                              o
     .4   .6    .8   1.0  1.2  1.4   1.6  1.8   2.0  2.2  2.4
                  AI/P WEIGHT RATIO

Figure 2. Phosphorus removal  by alum addition in O^

         activated sludge.
                         14

-------
 When alum addition to the 0*  process  improved  the  solids capture in the
 clarifier,  it also may have moderately improved  the  initial settling velocities
 for any given MLSS and wastewater  temperature.   The  initial settling velocities
 (Table 4) of  the MLSS fall within  the range of previously observed settling
 velocities  (Figure 3) for oxygen-activated sludge without alum addition.
 However,  in earlier work2  at the  EPA-DC Pilot Plant, the initial settling
 velocities of the  MLSS without alum addition during  similar seasons (November-
 February) tended to fall  within the lower portions of the observed range.  In
 the current study, the initial settling velocities of the MLSS with alum
 addition  clustered in the upper portion of the observed range.  Unfortunately,
 without a control  (parallel D£ process without alum  addition) for direct com-
 parison,  it was  not possible  to determine whether the apparent (compared to
 earlier observations) improvement  was related  to alum addition, and whether
 this improvement in initial settling  velocities  was  great enough to compensate
 for the increased  clarifier mass-loading caused  by the precipitated chemical
 solids.   In contrast to the apparent  increase  in the settling velocities of the
 MLSS,  the underflow solids concentration in the  clarifiers decreased with
 increasing  alum  dosage (Table 2).   (The thickening characteristics in the last
 half  of February and March should  not be considered  representative because of
 the heavy wasting  in mid-February).

 Finally,  filtration of the alum-C^ process effluent  through dual and multi-media
 filters was performed as  an additional compatibility study.  The filtration
 study, unfortunately,  was conducted during the operation with the highest Al/P
 dosage range  (2.66:1)  and did  not  correspond to  the  period of best alum
 addition-C>2 operation.  Thus,  the  solids concentration entering the filter were
 higher  than those  during  the most  efficient process  operation.  Two filter media
 were  employed  (Table 5),  a dual media and a multi-media.  In the multi-media,
 two different  coals,  one  of specific  gravity 1.4 and the other of specific
 gravity 1.6,  were  used to produce  a four media bed.  Laboratory Millipore
 filtration  (0.45u)  of  the effluents was performed for comparison with the in-
 depth pilot filtration.   In the  brief  tests, the filters were backwashed after
 a headless  of  3.18 meters (125  inches) of water  occurred across the filter.  The
 filter cycles  averaged approximately  10 hours with a backwash requirement of 15%
 of  the product volume.  The solids loading per filter cycle (in kg of solids per
 square meter  of  filtration area) ranged from 18.8 to 28.2 (.38 to .58 Ib of
 solids/ft^) and  were similar  to  typical loadings for filtration of other min-
 eralized  activated-sludge effluents in the pilot plant"' ^ .

 The filter  study revealed  filtration  performance (Table 6) on mineralized 02
 process effluent similar  to performances observed in earlier EPA-DC pilot
 studies-^ of mineralized  step-aeration activated-sludge effluent.  Although the
media specifications in the two  studies were different, the solids removals of
 60 to 75% in the current  study  compared well with the 62 to 78% removals of the
 earlier work^ on  the  alum-air activated sludge effluent.  With higher Al/P
ratios and  a lower effluent pH,  the  phosphorus residuals in the current study
were lower  than  the  average residuals reported in the earlier work   but were
 similar to  those residuals  observed in that earlier  work when the effluent pH
 of the air  system  was  in  the  6.4 to 6.5 pH range.
                                       15

-------
TABLE 4. SETTLING RATES
DATE
11/1/72
12/15/72
12/22/72
12/27/72
1/10/73
1/12/73
1/29/73
2/7/73
2/27/73
3/7/73
3/14/73
TEMP
(°c)
20.0
16.7
15.0
16.0
16.7
17.2
15.0
15.7
14.5
15.5
16.0
FOR 00 ACTIVATED SLUDGE WITH
SVI
(ml/gm)
46
41
--
37
42
51
51
48
51
71
54
MLSS
(mg/1)
5800
6540
8010
6650
7480
7340
5820
6870
5540
5740
4860
ALUM ADDI
ISV
(m/hr)
2.9
3.1
4.1
2.7
2.4
3.1
2.6
2.2
2.4
2.3
3.0

-------
     TABLE 5.   FILTRATION SYSTEM ON  ALUM-CL  SECONDARY  EFFLUENT
Media Specifications
Dual-media
Coal
Sand
Multi-media
Coal I
Coal 11
Sand
Ilmenite
Operating Conditions
Depth (m)
. 0.61
0.305

0.406
0.203
0.229
0.076

Size (mm)
1.24-1.44
0.6-0.7

1.5-1.6
1.0-1.1
0.4-0.5
0.2-0.35

Specific Gr
1.5
2.6

1.4
1.6
2.6
4.65

     Diurnal flow cycle,  peak  to  average                    1.6:1




     Average flow (m/min)                                   0.196




     Average cycle time  (hours)                             10




     Head  loss  at backwash  (m)                       . _     3.18




     Backwash requirement  (% of product)                    15




     Backwash rate (m/min)                                  0.81




     Surface wash rate  (m/min)                              0.12




     Filter  solids loading  kg/m2/cycle                     18.8-28.:
                                 17

-------
  5.00
u  1.00-
O
o
z
LU
to
  0.50-
   0.10-
  0.05-
                           oALUM  ADDITION
                           + STEP FEED
              EPA-DC  PILOT PLANT
              OBSERVED  SETTLING
              LIMITS (2)

               OXYGEN SLUDGE
              OBSERVED  SETTLING
                    LIMITS (8)
                   UNION  CARBIDE
                   5    lb
               MLSS CONCENTRATION (gm/l)
                       50
100
  Figure 3
Initial settling velocities of oxygen
MLSS as a function of concentration.
                        18

-------
       TABLE 6.  FILTER PERFORMANCE  ON  ALU.M-0  SECONDARY EFFLUENT
Pilot. Filters
Date
2/6/7*




2/7/74




2/14/74




Millioore



Sample
Inf. (mg/l)
Dual Eff. (mg/l)
/o Remova 1
7.'u Hi Eff. (mg/1)
% Removal
Inf. (mg/l)
Dual Eff. (mg/l)
% Removal
-Multi Eff. (mg/l)
/j Remova 1
Inf. (mg/l)
Dual Eff. (mg/l)
,°o Removal
Multi Eff. (mg/l)
% Removal
Filtration

Eff. P
°< Removal
SS
25
6
72
6
72
27
11
60
--
--
32
12
62
9
72

2/6/74
0.652
19
BOD
7.3
4.7
35
3.3
55
7.0
4.5
36
3.3
53
12.0
6.9
43
4.8
60




COD
36
29
19
19
47
35
25
29
19
46
54
32
41
32
41

2/7/74
0.74
20
P
0.805
0.365
55
0.346
57
0.926
0.405
56
0.150
33
2.06
0.531
74
0.346
83




Al/P
Ratio
3.95




4.13




1.99





2/14/74
1.72
17
                                   19

-------
With the snail data base of the current study, a meaningful comparison between
media types cannot be made.  However, comparison between the pilot in-depth
filtration and the laboratory Millipore filtration is appropriate.  Filtration
through the in-depth dual and multi-media filters removed more than 50% of the
residual P.  Filtration through the 0.45ji laboratory Millipore filters removed
only approximately 20% of the residual P.  These results confirmed similar
observations during extensive filtration studies  on the effluent from the
three-stage activated sludge pilot system in the EPA-DC Pilot Plant.   The in-
depth filtration improved the removal of phosphorus, either because of
increased precipitation and flocculation on the filter bed or because of
adsorption of the P on the Al (OH)., and other materials in the filter bed.
                                    20

-------
                                   SECTION  7

                               STEP-FEED  STUDIES


 In  the  step-feed  study,  the  operation  of the (^-activated  sludge process with
 an  equal  split  of  the  feed into  the  last three reactor  stages was initiated
 (Table  7)  in  late  June at a  steady flow  with a reactor  detention time of about
 1.85  hours and  with a  steady clarifier overflow rate of approximately 27.5 m/d
 (675  gpd/ft ).  Mineral  addition was not employed.  Data acquisition was ini-
 tiated  on  July  20,  1973.  The process  was  first operated at an F/M of about
 0.23  gm BOD5/gm MLVSS/day and at an  SRT  of 11 days.  Later the F/M was
 increased  to  0.32  gm BOD5/gm MLVSS/day.

 The important advantage  of the step-feed configuration  was the MLSS profile
 (Table  7)  through  the  reactor stages.  The MLSS decreased from nearly 10,000
mg/1  in the first  stage  to about 4,000 mg/1 in the last stage and averaged
 around  6,500  mg/1.   Thus, the step-feed  configuration produced a desirable and
modest  solids loading  (clarifier flux) of about 115 kg/d/m2 (23 lb/day/ft2)
 and a high average MLSS  without  a high flux loading to  the clarifier.

At the  operating SRT of  11 days,  the process exhibited  a low sludge production
 of about 0.5  gm of  solids/gm BOD,-  applied, with about half of the solids pro-
duction in the  waste sludge  stream and the rest in the  secondary effluent.  The
MLSS entering the clarifier  exhibited  typically excellent settling velocities
for summer operation (Figure 4).   The  initial settling velocities in the 15.25
cm diameter by  2.44 m  high column ranged from 5.3 to 8.3 m/hr (17.4 to 27.2
ft/hr)  (Table 8) and,  as typical of  warm-water settling rates, clustered in the
upper portion of the earlier observed  settling velocities (Figure 3).

The effluent  quality from the step-feed operation was excellent (Table 9).
With nitrification in  the process, an  allyl-thiourea inhibited BOD^ (0.5 mg/1
of allyl-thiourea) and an uninhibited  filtered BODtj were obtained on the final
effluent.   As in conventional plug-flow Oo-activated sludge1,  the process
operated in the step-feed configuration reduced the soluble BODcj to less than
3 mg/1  and  the  total residual  BOD5 (inhibited) to less  than 10 mg/1.  The
step-feed  process also efficiently removed COD (78 to 85%) and suspended
solids  (70 to 87%).  Without  alum  addition, the process removed from 17 to 42%
of the  total  P.  At  the high SRT,  the  system partially nitrified, converting
about 70%  of  the TKN to nitrate, and provided a total nitrogen removal of about
40%.  The nitrification and  C02 reduced the effluent pH to 6.3.   As expected,
the nitrification also reduced the effluent alkalinity.

The step-feed configuration,  because of treatment efficiency and clarifier
loading characteristics, is  especially well suited to the oxygen-activated
sludge process.  However, the key  to its application is the efficiency of

                                      21

-------
                                TABLE  7.  STEP-FEED, 0 -ACTIVATED SLUDGE OPERATING CONDITIONS
       REACTOR
to
ro
F/M
Detention gm BOD Average MLSS
Period Time SRT MLSS (mq/l)
1973 (hr.l
July 20-31
Aug. 1-31
Sept. 13-26
CLARIFIER AND
Period
1973
July r-0-31
Any. 1-31
Sept. 18-26
1.81
1.84
1.88
SLUDGE
Flow
Rate
(m3/d)
405
399
390
(qm MLVSS)(day) (days) (mq/l) (% Vol.) Staqe 1 Staqe 2 Staqe 3
0.26 10.7 6500 73 9800 6720 5180
0.23 11.5 6730 74 10,700 7060 5020
0.32 	 5830 74 8970 6040 4570
PRODUCTION
Clnrifier '_, * Underflow Solids Recycle . . . /
„ ,., Flux „.._ ,,,,-. n ' gm solids/gm
Overflow ,., SVI (A.) Rate 3 '^
(m/d) (kq/d/;;O (ml/q) Plow Tow Bro ("') Produced
28.0 120 50 2.06 1.70 53 0.49
27.5 115 37 2.15 1.84 51 0.50
27.0 102 49 2.16 1.78 42 	
Staqe 4
4310
4150
3760

BOD applied
Wasted
0.19
0.24
	

-------
  2.2




  2.0




   1.8




   1.6
1  12
O  l"*

tu

1  1.0




  0.8




  0.6




  0.4




  0.2
SLOPE  = 5.3 m/hr.
                                  MLSS,  3880mg/l


                                     TEMP., 26.7°C
            .25
       .50
1.25
                       .75      1.0

                      TIME (hrs)


Figure  4.   Typical step-O2  MLSS settling.
1.50
                           23

-------
to
                                 TABLE  8.   INITIAL SETTLING  VELOCITIES3   OF
                                             STEP-FEED,  DEACTIVATED  SLUDGE
                     SVI  (ml/g)           TEMP (°C)           MLSS  (mg/l)           ISV  (m/hr)
70
53
60
39
34
24.5
25.0
24.7
26.7
26 . 2
2620
4360
3860
3880
4510
6.9
5.5
8.3
5.3
5.5
                       aDynamic settling in 15.25 cm dia. by 2.44 m long settling column
                        mixed at 10 rph.

-------
                                 TABLE 9.  STEP-FEED, DEACTIVATED SLUDGE EFFLUENT QUALITY3
      CARBON AND SOLIDS
to
t-n
BODc, Filt. BODC ^^
Period In
1973 (mq/l)
July 20-31 	
Aug. 1-31 88.5
Sept. 18-26 111
PHOSPHORUS AND NITROGEN
PH
Period , ~ .
1973 In °Ut
July 20-31 6.9 6.3
Aug. 1-31 6.9 6.3
Sept. 18-26 7.0 6.3
Out Rem.
(mq/l) (%}
	
9.7 89
8.3 93

Alkalinity
In Out
(mq/l) (mq/l)
126 74
129 80
' 154 94
\j
Eff.
(mg/1)
—
2.8
2.4

Total
In
(mq/l)
5.78
5.51
7.45
In
(mq/l)
208
208
248

P
Out
(mq/l)
4.77
4.40
4.27
Out
(mq/l)
46
43
38

TKN
In
(mq/l)
20.2
20.6
24.5
Rem.
f
-------
utilization of the. Q2 gas feed to the process.  Prior to the step~feed study,
the equipment was completely renovated and the 02 recirculation compressors
were replaced.

During the summer operation with the new and renovated equipment, the system
exhibited unknown oxygen losses.  Finally in September, all leaks were elimi-
nated and brief oxygen balances were performed on the process.   Two approaches
to the oxygen balances were employed.  One approach was employed to compare
the measured 0~ in the inlet gas flow with the Oj in the outlet gas flow and
in the effluent stream (D.O.).  The second approach was employed to compare
measured inlet 02 with the oxygen used as measured by dissolved oxygen uptake
rates (Figures 5 and 6) in each of the process stages.  Both approaches to
the oxygen balance (Table 10) revealed about a 50% utilization  of the inlet 02.
Further work is needed to confirm these 02 balances and in particular to assess
the increase in mechanical energy input needed to decrease the  percent oxygen
in the exhaust gas.   However, if confirmed, oxygen usage of about 50% will
eliminate the step configuration as a practical alternative to  the 02 process
as practiced at the EPA-DC Pilot Plant.
                                     26

-------
2.0H

1.0
      0.0-
                                    SEPT. 25, 1973
                                MLSS = 8,115mg./l.
                                      STAGE NO.l
                                    UPTAKE = 96.8
                          RUN NO. 1
                           RATE = 11.64 mg02/l/hr
                                         gm MLSS
         RUN NO. 2
         RATE = 12.2 mgO2/l/hi
                       gm MLSS
                       23
                        TIME (min)
   O)
   £

   O
    •
   Q
6.0

5.0

4.0

3.0

2.0

1.0

0.0
                                     STAGE NO. 2
                                MLSS = 5400mg/l
                                   UPTAKE = 83.7
•RUN  NO.  1
  RATE = 15.4 mgO2/l/hr

                gm MLSS
         RUN NO. 2
         RATE =  15.5
                mg
                  gm MLSS
        01       2345
                        TIME (min)
Figure 5.  D.O. uptake as a function of  time  stage
           No. 1 and  2.
                         27

-------
    7.0

    6.0
= 4.0-
 O)
— 3.0-
  2.0-

  1.0-

    0
    1.0-
               DILUTE MLSS-
                 =1875 mg/l
                   RATE=15.45 mgO2/l/hr

                               gm MLSS
                                        SEPT. 25, 1973
                                        STAGE NO. 3
                                        UPTAKE=69.4
                                          mgO2/|/hr
                           ,MLSS=4,290 mg/l
                             RATE=16.88 mgO2/l/hr

                                         gm  MLSS
              1.0
                                    4.0
5.0
        2.0      3.0
          TIME (min)
                            STAGE NO.4
DILUTE MLSS 2015 mg/l      UPTAKE=57 2
      ;RATE=16.4mg02/l/hr   mgo2'/|/hr
      "^        gm MLSS
              MLSS=3560 mg/l
                  RATE=15.75 mgO2/l/hr
                              gm MLSS
              1.0      2.0      3.0      4.0      5.0
                       TIME (min)

Figure 6. D.O. uptake as a function of time stage No. 3 and 4.
                           28

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                            TABLE 10.  STEP-FEED, 0 -ACTIVATED SLUDGE OXYGEN USAGE
to
Time Period
Sept. 25*
09:28-17:09
12:27-15:35
Sept. 27b
10:03-18:24
15:10-18:24
°2
In
(kq)
33.6
12.9
49.0
21.2
Out
(kq)
16.6
6.3
25.6
11.4
°2
Usage
(o'\
\/°)
50
52
48
54
°9
D.O. Uptake
(kq)
18.0
7.4
21.1
8.5
02
Usage
(%}
54
57
44
40
                      a
                       Average % 0  in effluent gas 46%.
                      b           ^
                       Average % 0  in effluent gas 49%.

-------
                                  REFERENCES

  1.   Stamberg,  J.B,,  Bishop,  D.F, and Kumke,  G.  "Activated Sludge Treatment
      With Oxygen," AIChE Symposium Series 124,  Water 1971, 68.  25 (1972)

  2.   Stamberg,  J.B.,  Bishop,  D.F, Hais,  A.B.,  and Bennett, S.M., "System
      Alternatives in  Oxygen Activated Sludge/'  presented at the 45th Annual
      Conference of Water Pollution Control Federation,  Atlanta,  Georgia,
      October 1972.

  3.   "FWPCA Methods for Chemical Analysis of  Water and  Wastes/'  U.S.  Dept.
      of  the Interior,  Fed.  Water Poll. Control Adm.,  Cincinnati,  Ohio
      (November  1969).

  4.   Kamphake,L.,  Hannah, s.  and Cohen,  J., "Automated Analysis  for Nitrate  by
      Hydrazine  Reduction,"  Water Res., 1,  205  (1967)

  5.   Schaeffer,  R.B.,  et al.,  "Application of a  Carbon  Analyzer  in Waste  Treat-
      ment/' Jour.  Water Poll.  Control Fed., _37,  1545  (1965).

  6.-   Gales,  M.,  Julian E.,  and Kroner, R.,  "Method for  Quantitative Determi-
      nation of  Total Phosphate in Water,,"  Jour,  of Am.  Water Wks.  Assoc., 58,
      1363  (1966)

  7.   "Standard Methods  for  the Examination of Water and Wastewater."  12th ed.,
     American Public Health Association, New York (1965)

  8.  Linde  Division, Union  Carbide Corp.,  "Operating  Experiences  and  Design
     Criteria for Unox  Wastewater Treatment Systems." prepared for U.S. EPA
     Technology Transfer Program^  Design  Seminar  for Waste Treatment  Facilities,
     New York, New York, February 29-March 1, 1972.

  9.  O'Farrell,  T.P.,  and Bishop  S., "Filtration of Effluent from  Staged
     Nitrification-Denitrification Treatment/1 presented at the 76th  National
     Meeting of AIChE,  Tulsa,  March 10-13. 1974.

10.  Hais, A.B., Stamberg J.B, and  Bishop D.F,, "Alum Addition to Activated
     Sludge with Tertiary Solids  Removal/' AIChE  Symposium Series  145, Water
     1974,  71, 252 (1975).
                                       30

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                               PUBLICATIONS

Heidman, J. A., Bishop, D. F., and Stamberg, J. B., "Carbon, Nitrogen,
and Phosphorus Removal in Staged Nitrification-Denitrification Activated
Sludge Treatment," AIChE Symposium Series 145, Water 1974, 71, 264 (1975)
                                    31

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                                    TECHNICAL REPORT DATA
                             (Please read Instructions on the reverse before completing)
  1. REPORT NO.
   EPA-600/2-77-166
                                                           3. RECIPIENT'S ACCESSION-NO.
 4. TITLE AND SUBTITLE
   Alum Addition and Step-Feed
   Activated Sludge
    Studies   in Oxygen-
              5. REPORT DATE
                 September
1977 (Issuing Date
                               6. PERFORMING ORGANIZATION CODE
 7. AUTHOR(S)
   Dolloff F. Bishop,  James A.  Heidman, Richard C.
   Brenner, and John B.  Stamberg
                                                           8. PERFORMING ORGANIZATION REPORT NO.
 9. PERFORMING ORG -XNIZATION NAME AND ADDRESS
   Government of  the  District of Columbia
   Department of  Environmental Services
   EPA-DC Pilot Plant
   5000 Overlook  Avenue,  S.W., Washington, D.C.
                               10. PROGRAM ELEMENT NO.

                                    1BC611
                               11. CONTRACT/HHXHXNO.
                                68-01-0162
                     20032
 12. SPONSORING AGENCY NAME AND ADDRESS
   Municipal Environmental  Research Laboratory—Gin.,  OH
   Office of Research and Development
   U.S. Environmental Protection Agency
   Cincinnati,  OH  45268
                               13. TYPE OF REPORT AND PERIOD COVERED
                                Final Report - 10/72 to 10/73
                               14. SPONSORING AGENCY CODE
                                EPA/600/14
 15. SUPPLEMENTARY NOTES
   Project Officer:   Dolloff F.  Bishop (513-684-7628)
 16. ABSTRACT
 A plug flow, 02~activated sludge  process was operated with alum addition to remove
 phosphorus and with lime addition to prevent the process pH from decreasing below 6.4.
 The  02 reactor was operated at F/M ratios between 0.18 to 0.24 gm of  BOD5/gm of MLVSS/
 day  in a typical co-current 02~liquid contacting system.  The alum dosages  for the fiv
 steady-state operating periods increased from 84 mg/1 to 184 mg/1 was used  to maintain
 the  process pH at 6.4.  The pollutant removals from the primary effluent ranged from
 82 to  92% for BOD5 (7.4 to 19 mg/1 of residual 6005) and from 54 to 86%  for phosphorus
 (1.05  to 3.26 mg/1 of residual P).   The  optimum P removal occurred at a  1.8 to 1 aver-
 age  Al/P mole ratio with an average total residual P of 1.05 mg/1.

 In a second study, the 02 process  was operated in a step-feed configuration consisting
 of a sludge oxygenation stage followed by three stages of oxygen aeration with equal
 portions of the primary effluent  fed  to  each stage.  In typical operation,  the process
 with a F/M ratio of 0.23 exhibited  a  MLSS concentration profile in the four stages of
 10,700 mg/1;  7,060 mg/1; 5,020 mg/1;  and 4,150 mg/1.  The step configuration clearly
 reduced the solids loading to the  clarifier  and provided an average MLSS of more than
 6,500  mg/1.   The step operation produced excellent BOD5 removals (89% from  primary).
 The  02  usage in the step configuration was significantly less than the 90%  typically
 achieved  in co-current contacting.
17.
                                KEY WORDS AND DOCUMENT ANALYSIS
                  DESCRIPTORS
                                              b.IDENTIFIERS/OPEN ENDED TERMS
                                           c.  COSATI Field/Group
 *0xygenation
 *Activated Sludge  Process
  Sedimentation
  Aluminum Sulfate
  Sewage Treatment
  Calcium Oxides
 *Liquid Oxygen
Oxygen Consump-
  tion
pH Control
*0xygen activated  sludge
 Phosphorus removal
*Mineral addition
 Step-feed operation
 EPA-DC Pilot Plant,
   Washington, DC
 Dissolved Oxygen
   13B
13. DISTRIBUTION STATEMENT
      RELEASE TO PUBLIC
                 19. SECURITY CLASS (ThisReport)
                    UNCLASSIFIED
                           •21. NO. OF PAGES
                             40
                                              20. SECURITY CLASS (Thispage)
                                                 UNCLASSIFIED
                                                                        22. PRICE
EPA Form 2220-1 (9-73)
                                            32
                                                                    * U.S. GOVEBSMEKT PSIKU1IG OFFICE 1977- 75 7-0 56 /6 542

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