-------
The majority of the precipitation in the unit occurred during
the last feu hours before the runs were terminated. In both test
runs, mechanical problems caused the recovery to soar to undetermined
levels (probably greater than 90 percent) before the unit shut down
and thus the brine was very concentrated and precipitation occurred.
As calcium sulfate is the first salt to exceed solubility, it was
expected that the precipitate would be largely calcium sulfate. The
results in Table 17 confirm this conclusion.
However, this predominance of CaSO deposition may not be repre-
sentative of what occurred during successful operation. The possi-
bility of ferrous iron fouling cannot be ruled out nor can it be
substantiated by these results.
Contrasting the salt rejections at Arkwright with those at Morton,
the rejections at Norton were slightly higher in most cases. This
difference in rejection rates was due to the high ionic concentration
at Arkwright whose higher osmotic pressure resulted in less product
flow while the salt flow remained essentially the same. This con-
clusion was valid since osmotic pressure is directly related to
ionic concentrations and increases in ionic concentrations elevate
osmotic pressure.
In conclusion, it does not appear that RO would be a feasible
method for treatment of water of this quality based upon the problem
of membrane fouling which severely limited recovery (50 percent)
resulting in disposal of an equal volume of brine for each gallon
of water reclaimed.
EBENSBURG U K FERROUS IRON SPIRAL-WOUND STUDY
A ferrous iron test site with concentrations more typical of AMD
commonly encountered was located near Ebensburg, Pennsylvania, at
the 32-33 discharge of Bethlehem Mines Corporation Cambria Division.
The k K spiral-wound test system was installed there in July 1970.
The study included tests to determine if iron fouling could be con-
trolled by pH adjustment, i.e., the lower the pH, the less liklihood
of iron precipitation.
53
-------
A new, improved version of Gulf Environmental System's standard
flux, high-selectivity module uas used in this Ebensburg study. In
these modules, the membrane uas cast directly upon the backing mate-
rial and the old glue joints uere eliminated. The glue joints may
have contributed to small "leakage" problems in the past and the
manufacturer felt that their elimination should insure high rejec-
tion rates.
The system flouj arrangement uas the same as that at Arkuright
(Figure 11) except for acid injection which uas used during this
study. Osmotic pressure uas assumed to equal ID psi per 1,000
micromhos of conductance, tilater quality of the Ebensburg site uas
similar to that at Morton (except for ferrous iron).
Four tests uere made during this study. These were:
Test Number One: A 191 hour, 80-85 percent recovery, recycle
brine run utilizing injection of sulfuric acid into the feed water to
louer the pH from pH 3.6 to pH 2.5. Acid injection uas used since it
uas feared that ferric iron might precipitate at pH 3.6. The amount
of acid injected uas gradually diminished touard the end of the test.
The last module in tube 3 uas removed at the end of the test and re-
turned to Gulf Environmental Systems for post mortem analysis.
Test Number Tuo: An 86 hr, 80-85 percent recovery, recycle
brine run with no pH control of the feed (i.e., no acid injection).
Test Number Three: An 18 hr, 80-85 percent recovery, recycle
brine run utilizing injection of sodium hydroxide to increase the pH
of the blended feed (blended feed = raw feed plus recycled brine;
blended feed is the uater actually entering the RO unit) to pH 3.6.
The purpose of this test uas to simulate the rau uater pH to deter-
mine if ferric iron precipitation uould occur in a unit uith no
brine recycle.
Test Number Four: A 3k hr, 50-55 percent recovery run uithout
brine recycle and no pH control. A neu module had been installed in
tube 3 at the start of this run. After the test, the module uas re-
-------
moved and returned to Gulf Environmental System for post mortem
analysis. This test investigated the fouling rate at louer re-
coveries.
Test Number One
As the pH of the AMD at Ebensburg was 3.6, the possibility of
ferric iron precipitation uas feared. Sulfuric acid uas, therefore,
injected automatically into the uater before it entered the RQ unit
in order to louer the pH to 2.5. The test run lasted 191 hr and the
amount of acid injected uas gradually diminished toward the end of
the run. The recovery during the test uas maintained near 8*4 per-
cent by recycling a portion of the brine into the feed to the unit.
As tube 3 ur-s subject to the most polluted water, it uas more
prone to fouling than tubes 1 and 2. As shoiun in Figure 12, the
pressure drop (AP) across tube 3 after 100 hr of operation had
increased significantly, thus indicating membrane fouling. The
recovery uas then reduced for three hours in an effort to remove
the fouling. The flush uas successful in restoring the AP across
tube 3 to normal values. Significantly, theAP across tubes 1 and
2 decreased during the run uhile tube 3 increased, indicating that
the-fouling uas a concentration-related phenomenon.
The flux history of the run is shoun on a linear basis in Fig-
ure 13. Very little fouling uas observed in tubes 1 or 2 as their
log-log slopes uere -0.0^3. An excessive flux decline uas observed
in tube 3. A rapid change in log-log slope for tube 3 occurred
after approximately ^0 hr of operation on the Ebensburg uater.
It is felt that the tube 3 flux loss mas due to calcium sulfate
fouling. Although acid injection uas diminished as the run pro-
gressed, very little change occurred in the tube 3 pH as shown in
Table 18. Thus, the decrease in acid injection probably had no
significant effect on tube 3 behavior.
55
-------
U1
en
75
O Tubes 1 & 2
Tube 3
50
25
50
150
100
ELAPSED TIME, hours
Figure 12. (AP) Pressure drop across tubes during Test Number One.
200
-------
0)
C
o
o
o
TJ 17.5
C
o
@;15.5
x
o
TJ
~ 13.5
o
u>
X
^ 11.5
9.5
o Tube 1
A Tube 2
D Tube 3
700
cs
E
00
to
TJ
C
O
u
o
CM
600
X
0)
500^
tt
LU
t—
<
- 400
50
100
ELAPSED TIME, hours
150
200
Figure 13. Membrane performance during Ebensburg test at 84 percent recovery.
-------
Table 18. BLENDED FEED AND BRINE pH'S AT EBENSBURG
Elapsed
time, hr
0-28
28-57
57-96
96-100
100-191
Blended
feed pH
2.7
2.75
2.8
3.2
3.1
Elapsed
time, hr
0-100
100-191
Brine
(tube
2.3
2.6
pH
3)
On the log-log graph, there appeared to be a slight tendency
for the tube 1 flux values to tail off from the linear log-log
slope of -0.0^3 between hours 100 and 191. Unfortunately, the run
did not continue long enough to substantiate this suspicion. If
some fouling uere occurring in tubes 1 and 2 during that time period,
it would likely have been due to iron precipitation as the pH (Table
18) had increased to 3.1 during that portion of the test.
A module mas removed from the downstream end of tube 3 at the
end of the test and returned to Gulf Environmental Systems for post
mortem analysis. Sleigh reported the presence of a white flaky
precipitate in the module:
"Analyses of this material showed it to be 23.7
percent calcium, 55.1 percent sulfate, and 22.6
percent loss of weight at 600° C. The theoret-
ical amount of CaSO^ in gypsum (CaSO,.2H 0) is
79.1 percent; therefore, this material was almost
pure gypsum. The precipitate could easily be
washed from the membrane which is what takes
place in the unit when the recovery level is
lowered."
No tests were made to determine the presence of iron.
Table 19 presents the physical data for the test run and Table
20 shows the chemical analyses. Salt rejections were uniformly
greater than 99 percent on all multivalent ions.
58
-------
Table 19. OPERATING PARAMETERS FOR TEST NUMBER ONE AT EBENSBURG, PENNSYLVANIA
m
Average recovery, percent
Average feed rate, gpm
Average brine flout rate, gpm
Average recycle brine flou rate, gpm
Average temperature, °F
Average feed pressure, psi
Average product flou rate, gpm
Normalized to 50°F, gpm
Normalized to 77 °F, gpm
83.6 Avg. 85.7 Max. 81.2 Min.
3.57
0.59
3.79
63.6 Avg. 67.5 Max. 59.0 Min.
399.2
2.98
2.32
3.72
2
Average flux rate, gal/ft/day @ 50°F and 400 psi net 7.44
Average flux rate, gal/ft2/day @ 77°F and 400 psi net 11.90
Maximum brine/product flou ratio 19.6:1
Minimum brine/product flou ratio 7.5:1
Dates of test : July 30 - August 7, 1970
Length of run : 191 hours
Number of shutdowns: 0
Note: To convert flux (gal/ft2/day @ 400 psi and 77°F) to Iiters/m2/day @ 2758 kN/m2 and 25° C,
multiply by 40.67; to convert gallons per minute to liters/second, multiply by 0.063; and to
2
convert psi to kN/m , divide by 0.145.
-------
Table 20. CHEMISTRY ANALYSES FOR TEST NUMBER ONE WHERE AVERAGE RECOVERY = 83.6%
en
o
pH
Conductivity
Acidity
Calcium as Ca
Magnesium as Mg
Aluminum
Total iron
Ferrous iron
Sul fates
Dissolved oxygen
Raw
feed
3.6
1500
380
190
5k
32
135
100
1640
2.0
Acidified
feed
3.0
1825
450
190
54
32
135
100
1620
—
Blended
feed
2.7
5100
1270
600
190
100
430
310
5100
•~
Brine
2.5
6900
2360
920
340
180
730
540
9300
2.0
Product
4.1
92
56
1.2
0.4
0.9
1.7
<2
14
2.0
Rejections*
98.2%
95.6%
99.8%
99.8%
99.1%
99.6%
99.4%
99.7%
~
All units are mg/1 except for conductivity (Mmhos/cm) and pH.
•Rejection equals
Blended feed concentration-product concentration
Blended feed concentration
X 100,
-------
Test Number Two
The injection of sulfuric acid to control the influent pH was
not used in this test as it was observed that, at 8Q-S5 percent
recovery, the recycled brine lowered the pH of the resulting "blended
feed" from pH 3.6 to pH 3.1.
This test was plagued with shutdowns. In a total run time of
86.3 hr, the longest continuous run was 22.5 hr and the longest
continuous period of data available was for only 17.3 hr. The shut-
downs were all caused by pump problems.
Table 21 shows the flux andAP value for Test Number Two.
Each accidental shutdown acted as a flux rejuvenator. Planned
full pressure shutdowns have long been used at Morton to dislodge
precipitates and restore membrane performance. In essence, each of
these accidental shutdowns served to clean and relax the membrane.
Considering the data between shutdowns as individual runs, the
flux values in most cases decreased as the run progressed. As in
Test Number One, the flux decline in tube 3 was significantly
greater than the decline in tubes 1 or 2.
The AP value over the entire test run did not change appreciably
for tubes 1 and 2 but did show a continuous increase across tube 3.
This was analogous to the results of Test Number One.
Flux rates for tubes 1 and 2 were greater at the end of the test
than at the beginning. The tube 3 flux decreased 9.2 percent over
the entire run.
Overall, there was significantly less fouling in Test Number
Two than in Test Number One, due to the shutdowns which acted as
precipitation removers.
The physical data for Test Number Two are shown in Table 22 and
the chemical analyses are given in Table 23. As in Test Number One,
the salt rejections of all multivalent ions were greater than 99
percent.
61
-------
Table 21. FLUX AND AP VALUES FOR EBENSBURG TEST NUMBER TWO
Elapsed
Time
(Hours)
Flux
Tube
1
Flux
Tube
2
Flux
Tube
3
AP
Tubes
1&2
AP
Tube
3
(psi)
(psi)
0.7
2.8
5.9
22.5
22.9
24.7
27.8
45.0
46.5
51.0
62.5
63.5
66.0
68.5
69.0
70.4
72.5
86.3
14.95
14.73
14.50
15.53
14.74
14.62
15.47
14.56
14.28
15.35
14.98
14.31
15.32
14.95
15.59
14.92
14.70
14.58
15.40
14.71
14.71
15.32
14.41
14.24
15.32
14.95
14.28
15.19
14.82
15.35
15.25
15.02
15.02
Pump Failed
15.63
14.91
14.68
Pump Failed
15.44
14.15
13.84
Pump Failed
14.53
14.23
13.18
Pump Failed
14.37
13.74
13.85
4.75
4.70
4.75
4.75
4.75
4.75
4.75
4.75
4.75
4.70
4.70
4.70
4.70
4.70
4.70
8.70
8.75
8.80
8.90
8.90
8.90
8.90
8.90
8.90
8.90
9.10
9.20
9.2
9.3
9.8
M.UUB. riux expresseo as gal/ftVday 8 77"F and 400 psi net. To con-
vert flux (gal/ft2/day 8 400 psi and 77° F) to Iiters/m2/day 8 2758
kN/m and 25° C, multiply by 40.67 and to convert psi to kN/m2, di-
vide by 0.145.
62
-------
Table 22. OPERATING PARAMETERS FOR TEST NUMBER TWO AT EBENSBURG, PENNSYLVANIA
en
Average recovery, percent 84.0 Avg.
Average feed rate, gpm
Average brine flow rate, gpm
Average recycle brine floiu rate, gpm
Average temperature, °F 63.3
Average feed pressure, psi
Average product flow rate, gpm
Normalized to 50°F
Normalized to 77°F
2
Average flux rate, gal/ft /day @ 50°F and 400 psi net
2
Average flux rate, gal/ft/day @ 77°F and 400 psi net
Maximum brine/product flow ratic
Minimum brine/product flow ratio
84.5 Max. 82.8 Min.
3.81
0.61
3.29
60.0 Min. 68.0 Max.
400
3.20
2.42
3.87
7.74
12.38
13.4:1
6.8:1
Dates of test : August 17-21, 1970
Length of run : 86.3 hours
Number of shutdowns : 4
Note: To convert flux (gal/ft2/day @ 400 psi and 77°F) to Iiters/m2/day § 2758 kN/m2 and 25°C,
multiply by 40.67; to convert gallons per minute to liters/second, multiply by 0.063; and to
2
convert psi to kN/m , divide by 0.145.
-------
Table 23. CHEMISTRY ANALYSES FOR TEST NUMBER TWO WHERE AVERAGE RECOVERY = 84.0%
en
PH
Conductivity
Acidity
Calcium as Ca
Magnesium as Mg
Aluminum
Total iron
Ferrous iron
Sulfates
Dissolved oxygen
All units are mg/1
(a)
Rpipr-hinn onualc
Raw Blended
feed feed
3.6 3.1
1470 4000
385 1160
210 650
63 200
37 110
150 460
98 280
1700 5200
2.0
Brine
3.0
6800
2150
1200
390
220
870
550
10,000
2.0
Product
4.6
85
58
1.8
1.1
1.1
1.9
<2
23
2.0
Re.iections(a)
97.9%
95.0%
99.7%
99.4%
99.0%
99.6%
99.3%
99.6%
^
except for conductivity (Mmhos/cm) and pH.
Blended feed concentration-product
concentration ., ,.
nn_
Blended feed concentration
-------
Test Number Three
Uithout brine recycle or acid injection, the RD unit would have
to treat pH 3.6 AMD at this site. It was the intent of Test IMumber
Three to simulate pH 3.6 influent conditions to the ^ K unit by in-
jecting sodium hydroxide to increase the pH of the blended feed.
The point of injection was highly critical in this application.
Referring to Figure ID, if the IMaOH were injected into the blended
feed, and overtreatment occurred, the ferric iron mould precipitate
directly in the RO unit. To protect the RO unit, the (MaOH was in-
jected into the raw feed prior to the sand filters. As the recycled
brine louered the blended feed pH from pH 3.6 to pH 3.1, the NaDH
increased the raw feed pH to counteract the effect of the recycled
brine. This meant the raw feed must be increased to approximately
pH 3.9 to obtain the desired result. At pH 3.9, however, the ferric
iron rapidly precipitated in the sand filter. The clogged sand fil-
ter prevented water flow to the unit so the test was discontinued.
The collected data were not sufficient to establish any definite trends.
Test IMumber Four
By eliminating brine recycle, the pH conditions which Test IMumber
Three uas trying to produce were achieved. With no recycled brine,
the raw AMD uas fed directly into the RD unit at pH 3.6. Unfortu-
nately, without the use of brine recycling, the small ^ H unit uas
limited to approximately 55 percent recovery.
Figure 1U shows the AP and flux history for the 3k hr, 50-55
percent recovery test. The AP remained constant throughout the
test run. Flux values, though someuhat erratic, uere identical for
tubes 1, 2, and 3. Flux history (Figure 1^+) did not indicate foul-
ing in any of the tubes. This was quite different from the readily
app3rent fouling seen in Tests IMumber One and Two. Peaks in the
flux value graph all occurred during periods of lowest water temper-
ature which indicate some discrepancies may exist betueen the manu-
facturer's temperature-flux normalization curve and the behavior of
the Ebensburg water.
65
-------
a.
° 7.0
Q
0)
3
0)
k
O.
o.
<
5.0
X
o
TJ
» a
^ O
~D °
O) "**
20-°
10.0
n-EHD-
-QO—a-
-Q
O TUBES 1&2
D TUBE 3
O
0
O
Q
i—
U
I
to
O TUBE 1
A TUBE 2
D TUBE 3
30
90
E
Z
40
30
D CS
~O e
800 « z
a> °°
«. f>
600
T3
C
u
Of o
400
60
ELAPSED TIME, hours
Figure 14.
Membrane performance andAP history for Ebensburg RO Test Number Four at
50 percent recovery
-------
Physical data for Test Number Four are presented in Table 24
and the chemical analyses are given in Table 25. Salt rejections
(Table 25) uere greater than 99 percent on all multivalent ions
except aluminum.
The downstream module in tube 3, which had been installed at
the beginning of Test Number Four, uas removed and a post mortem
analysis made. Sleigh reported that the module had been damaged
during shipment. He observed some iron present on the membrane
surface but uas unable to quantify it. There was no calcium sulfate
present on the membrane.
Discussion of Four Ebensburq Tests
At this site, it uas seen that pretreatment of the feed to louer
the pH uas not necessary for short-term tests as long as the pH uas
near 3.1 and/or the recovery uas near 50 percent.
Product uater quality, though uniformly good, uould require
slight addition of lime and filtering to be of potable quality.
As the fouling at 85 percent recovery could be removed success-
fully by a ueekly 3 hr lou-recdvery flush, fouling uould not pro-
hibit operation at that recovery level. The flux at 50 percent
recovery (Test Number Four), however, uas roughly 15 percent greater
than the flux during the 85 percent recovery runs (Tests Number One
and Tuo). Therefore, obvious improvements in membrane performance
can be obtained by operating belou the CaSO, fouling level.
Table 26 compares the results of the first Ebensburg test uith
^
those of REX Chainbelt at Mocanaqua. The spiral uound unit uas
operating at Ebensburg under more severe conditions in terms of
concentrations than the tubular unit at Mocanaqua, yet it produced
significantly superior results in terms of flux stability and product
quality. Due to the apparent success of the spiral unit at Ebensburg,
it uas not possible to determine if the fouling observed at Mocanaqua
uas peculiarly due to the tubular RO system or uhether some unknoun
characteristic of the Mocanaqua uater uas responsible.
67
-------
Table 2^. OPERATING PARAMETERS FOR TEST NUMBER FOUR AT EBENSBURG, PENNSYLVANIA
Average recovery, percent 53.2 Avg. 5*4.8 Max. 52.3 Min.
Average feed rate, gpm 6.33
Average brine flow rate, gpm 2.97
Average recycle brine flow rate» gpm 0
Average temperature, °F 60.2 Avg. 5^.0 Min. 63.0 Max.
Average feed pressure, psi ^01.1
Average product flow rate, gpm 3.36
Normalized to 50°F, gpm 2.78
g Normalized to 77°F, gpm k.k5
Average flux rate, gal/ft /day § 50°F and **00 psi net 8.90
Average flux rate, gal/ft2/day @ 77 °F and MDO psi net 1*«.2<*
Maximum brine/product flout ratio 8.7:1
Minimum brine/product flow ratio 5.5:1
Dates of test : August 31 - September U, 1970
Length of run : 93.5 hours
Number of shutdowns : 2
Note: To convert flux (gal/ft2/day @ UQO psi and 77°F) to Iiters/m2/day @ 2758 kN/m2 and 25°C,
multiply by U0.67; to convert gallons per minute to liters/second, multiply by 0.063; and to
2
convert psi to kN/m , divide by 0.1^5.
-------
Table 25. CHEMISTRY ANALYSES FOR TEST NUMBER FOUR WHERE AVERAGE RECOVERY = 53.2%
en
PH
Conductivity
Acidity
Calcium as Ca
Magnesium as Mg
Aluminum
Total iron
Ferrous iron
Sul fates
Dissolved oxygen
Ram feed
3.6
1160
390
160
51
30
130
96
1300
2.0
Brine
3.k
2160
770
330
110
61
250
210
2900
2.0
Product
<*.8
27
2k
1.1
0.3
1.1
O.i»
1.0
1.0
Rejections*
97.7%
93.956
99.3*
99.<»%
96.3%
99.5%
99.0%
99.9%
All units are mg/1 except for conductivity (Mmhos/cm) and pH.
-n . .. , Feed concentration-product concentration v lnn
*Rajection equals » . nnnnon+£U
-------
Table 26. COMPARISON OF MOCANAQUA AND EBENSBLJRG RO TEST RESULTS
Operating Parameters
Location
Investigator
Type of unit
Date of test
Length of test
Flux loss in 190 hours
Mocanaqua
Rex Chainbelt
Tubular
1969
813 hours
^40 percent (total unit)
Operating recovery (190 hours) :«70 percent
Ebensburg
EPA & Gulf Environmental Systems
Spiral-wound
1970
191 hours
zz25 percent (total unit)
:»84 percent
Chemical Parameters
Mocanaqua
Feed Product
pH
Acidity
Calcium
Sulfates
Total iron
Ferrous iron
Dissolved oxygen
Magnesium
3.6
—
140
790
100
100
4.9
100
4.1
—
2.8
36
3.7
3.7
—
1.9
Ebensburg
Feed Product
3.6
380
190
1640
135
HJO
2.0
54
4.1
56
1.2
14
1.7
>2
—
0.4
All units are mg/1 except for pH.
-------
Plans ijjere made to take the spiral RD unit to the Mocanaqua site
in the spring of 1971 to further investigate the situation.
NORTON FERRIC IRON LONG-TERM SPIRAL-WOUND STUDY
Following the Ebensburg study, the k K spiral unit was returned
to Norton for a long-term uinter study before going to Mocanagua in
the spring of 1971.
This Norton study lasted 3,013 hr at 73 percent recovery. The
flow arrangement (Figure 10) uas the same as previous studies except
that no pH control uas used. Neu high-flux modules uiith membrane
cast directly on the backing material were used for this test. One
of the major problems prior to this investigation uas the unreliabil-
ity of high pressure pumps to operate on AMD. A Gould MB 13600,
ceramic-stainless steel, multi-stage, centrifugal pump uas tested
on this study and performed flawlessly.
Flux history for the 3,013 hr test is shoun on a log-log basis
in Figure 15. Tube 3, uhose performance uas usually belou that of
tubes 1 or 2 due to its higher concentrations, exhibited superior
performance to tubes 1 and 2. Log-log slope changes occurred in
all tubes after approximately 300 hr. Until that time, tube 3 had
followed a log-log slope of -0.031 and tube one's slope uas -0.058.
Several flushing techniques, which are individually discussed
later, uere successful in restoring flux to values in excess of
those predicted by the initial slope. However, rapid flux losses
immediately recurred following each flush. The loss in tubes 1
and 2 was more severe than tube 3's loss. At the end of 3,013 hr,
tubes 1 and 2 had each lost 58 percent of their initial flux and
tube 3 had lost 38 percent.
The operating parameters for this study are given in Table 27
and chemistry analyses are presented in Table 28.
The data in Table 27 provide a possible explanation for the poor
performance of tubes one and two in respect to tube 3. Brine/prod-
uct flow ratios for this study were extremely low in general and
71
-------
X]
I\3
100
8O
70
6O
50
40
3O
o
c
S.20
o
o
•o
u.
o
£ 10
8
7
6
"X.
1 5
o
-o
-5 4
at
1
© TUBE THREE
• TUBE ONE
NOTE : 1 gal./ft2/day = 40.7 Iiter/m2/day
77°F = 25°C
600psi = 4138 kN/m2
I
I I I I ! I I
I
_L
I
10 2345 6789100 2 345 67891000 20003000
ELAPSED TIME, hours
Figure 15
Flux trends for Norton 3000 hour spiral-wound R.O. study at 13 percent recovery
-------
Table 27. OPERATING PARAMETERS FOR 3000 HR 4K NORTON STUDY AT 73
PERCENT RECOVERY
Parameter
Raw water feed flow
Product water flow
Brine water discharged
Brine water recycled
Minimum brine/product flow ratio
Maximum brine/product flow ratio
Water recovery
Recovery of blended feed
Feed pressure
Feed temperature
Tube one flux gal/ft/day @
2
Tube two flux gal/ft /day @
Tube three flux gal/ft2/day @
Unit
gpm
gpm
gpm
gpm
ratio/module
ratio/module
percent
percent
psig
op
77°F & 600 psi net
77°F & 600 psi net
77°F & 600 psi net
Value
5.00
3.6*+
1.36
1.46
2.8:1
6.6:1
72.8
56.3
600.2
54.4
17.43
17.25
20.41
Length of run
Date of run
hours 3012.6
November 16, 1970 - April 13, 1971
All values are means from 130 data sets.
Note: To convert flux (gal/ft2/day @ 600 psi and 77°F) to liters/
m2/day @ 4138 kN/m2 and 25°C, multiply by 40.67; to convert gallons
per minute to liters/second, multiply by 0.063; and to convert psi
to kN/m2, divide by 0.145.
73
-------
Table 28. NORTON UK 3000 HR CHEMICAL ANALYSES
Parameter
Raw feed
Blended feed
Brine
Product
Rejections
pH
2.9
2.7
2.5
3.9
Cond.
970
1600
2900
77
95.2%
Acidity
440
660
1600
22
96.7%
Cal Mg
120 39
180 71
420 140
1.1 .40
QQ /. Q£ QQ /.Q£
77«H^u 77*H7D
Fe
130
210
480
1.1
99.5%
Al
40
63
150
1.5
97.6%
*\
680
1100
2600
1.2
99.9%
„ . ., . Blended feed concentration-product concentration v inn
Rejection equals tiionn0H POOH mnnont^tinn X 10D
Blended feed concentration
All units are rog/1 except for conductance (micromhos/cm) and pH.
-------
at a minimum in tubes one and two (b/p minimum ratios of
2.8:1). The b/p ratio in tube 3 was significantly higher with
a maximum ratio of 6.6:1. It was felt that the lou brine/product
ratios did not provide sufficient turbulence in the brine stream
in the modules and thus did not effectively control boundary layer
precipitation.
Salt rejections (Table 28) mere uniformly above 99 percent on
all multivalent ions except aluminum.
Near the end of the test, copper sulfate uas injected directly
into the rauj feed water to determine the capability of the membrane
to reject copper. Concentrations of copper in the feed were varied
from 2,8 to ^ mg/1 resulting in blended feed concentrations from
4.*i to 60 mg/1. The membrane rejected an average of 99.5 percent
(based upon blended feed), yielding product copper levels below
D.16 mg/1 and brine copper concentrations up to 150 mg/1 at 75
percent recovery.
The severe fouling which occurred during this study afforded an
opportunity to investigate the effectiveness of various flushing
techniques. The flux history through 2,500 hr is shown on a linear
basis in Figure 16 to illustrate more clearly differences in flush
results.
The type of flush and its success in fouling removal should yield
some insight into the nature of the fouling. A list of the flushing
tried and their expected results follous:
1. Low-recovery Flush - Mainly scours the membranes due to
higher brine velocities and corresponding increases in
turbulence. Should remove some loose precipitation
such as flocculated ferric hydroxide or calcium sulfate.
May dislodge particulate matter. Mainly a physical
flushing technique.
2. Acidified Product Flush - Product water is stored and
acidified to pH 2.5 and then pumped through the RO unit.
75
-------
-o
en
»S
at
X
- 1000
15
NOTES
1 ACIDIFIED PRODUCT FLUSH AND
UNIT SHUT DOWN FOR ONE WEEK
DUE TO FLOODING
2 LOW RECOVERY FLUSH AND UNIT
SHUT DOWN OVER WEEKEND
500
1500
H800
u
o
CN
O
2
<
E
oo
CO
o
T3
CN
500
2000
1000
ELAPSED TIME, HOURS
Figure 16
Membrane performance during 4K reverse osmosis 3000-hr study at Norton
-------
This type flush should chemically redissolve those min-
erals uhich are acid soluble (i.e., iron, aluminum, cal-
cium, and some calcium sulfate) if the fouling is not
too severe before the flush is attempted.
3. BIZ flush - The catalytic action of enzymes should
mainly remove organics by breaking doun protein-contain-
ing materials. BIZ also contains uetting agents that
should aid in the resolubilization of precipitates and
phosphates that should be quite effective in sequestering
iron, calcium, and magnesium as well as in emulsifying
oils.
4. Shutdouns - Immediate depressurization should tend to
dislodge precipitates that have been held against the
membrane by pressure and RQ floiu through the membrane.
During long periods of depressurization, the membrane
tends to relax and the effects of compaction are reduced.
Also, normal osmotic flow (from product side into brine
side) takes place during this period and should tend to
dislodge precipitates from the brine side of the membrane.
Although all the flushes attempted (Figure 16) ujere successful
in improving flux, the most dramatic increase occurred using a tuo-
step flush. First, the unit uas flushed with acidified product
water, and then it was shut doun for one ueek because of flooding
uhich overloaded the filtration equipment. This accidental combina-
tion acid flushr-shutdOLjn at 725 hours elapsed time significantly im-
proved flux. Houjever, after each flush, flux again rapidly declined.
As each of the previously mentioned flushes were successful, the flux
decline uas attributed to a combination of compaction, iron fouling,
and organic deposition.
Samples were taken during the citric acid flush at 2,500 hours
elapsad time. Recovery during the flush uas maintained at 50 per-
cent so the brine concentrations should have been tuice that of the
rau feed. The resulting analyses indicated that the brine contained
77
-------
twice as much magnesium, aluminum, and sulfate as was in the acidi-
fied feed (normal far 5D percent recav/ery); however, eleven times
more iron and three times more calcium were in the brine than in the
feed. The predominance of iron in the flush brine indicated iron
precipitation was the major inorganic fouling mechanism.
A module was removed from tube 1 after 3,013 hr of operation at
Morton and dissected for membrane deposit analyses. An algal slime
covered the outside of the module. The membrane removed had an ob-
vious coating on it which, from its red-brown appearance, was tenta-
tively identified as ferric hydroxide.
For chemical analyses, the membrane was cut into small rectangles
(approximately 0.79 cm x 1.18 cm br 2 in x 3 in). Various reagents
were used to attempt to dissolve the coating from the membrane
patches. Table 29 lists the reagents used and chemical analyses of
the resulting solution. Initial analyses were made on each of the
reagents to determine background levels and to identify possible
interferences ujith the analytical procedures. Membrane patches ujere
weighed before and after immersion in the dissolving solution in an
attempt to correlate the resulting concentrations to a gravimetric
reference base (weight of coating). In most cases, however, the
solutions dissolved the membrane as well as the coating and only the
fabric backing material remained; therefore, the gravimetric refer-
ence base was ineffective as it was not possible to ascertain the
amount of membrane removed when only partial membrane destruction
occurred. The membrane coating appeared to consist mainly of iron
and-sulfate (Table 29). Presence of sulfate without calcium was not
completely understood.
Samples of the membrane were sent to Rex Chainbelt and Gulf
Environmental Systems for analysis. Mason of Rex Chainbelt found
two distinct layers of fouling material on the membrane:
"The first layer closest to the membrane was an iron
oxide coating. The second layer was a clay-like sub-
stance which was approximately 65 percent organic ma-
78
-------
Table 29. CHEMISTRY ANALYSES OF COATING MATERIAL ON 4K REVERSE OSMOSIS MEMBRANE
UD
Sample
designation
Blank
Stannous chloride
Blank
Sodium hydrosulfite
Blank
Citric acid
Blank
Hydrochloric acid
Blank
Phosphoric acid ,, ^
Stannous chloride,. J
Stannous chloride /•. •»
Sodium hydrosulfite^ x
Sodium hydrosulfite
Citric acid
-------
terial. This second layer adhered to the mem-
brane very loosely, and was easily removed hy
slight egitation. The ease of removal may have
been due to the handling of the membrane when
removed from the pressure vessel and shipped
to Milwaukee. The membrane flux, tested with
both layers of fouling material, was 12.7
gel/ft^ dav at U15 psi and 77° F. Salt rejec-
tion was approximately 96 percent sodium chlo-
ride. The membrane was flushed with R 2 mt.
percent of sodium hydrosulfite (IMa^S,-^ ) in
water. The pH of this solution was approxi-
mately 6.0. This chemical solution provided
a strong reducing environment which converted
the ferric iron to soluble ferrous iron, and
thus allowed cleaning of iron oxides from the
membrane. This cleaning can generally be effected
with a two-hour flush. After cleaning by the
above procedure, the membrane had a flux of
16.6 gal/ft? day at £*15 psi and 77" F. The salt
rejection remained unchanged at 96 percent, and
therefore the membrane surface was not damaged.
It should be noted that the second layer of
fouling material was not dissolved by the sodium
hydrosulfite solution, and therefore must be re-
moved by other methods, such as normal osmosis
flushing, enzyme solutions, and high velocity
flushing. "
1^
Sleigh reported the analysis of the coating material to be fer-
ric hydroxide and mud.
Since the product mater was not of potable quality, a feasibility
test was made for lime neutralization to increase pH and remove resid-
ual iron.
80
-------
During the test, product from the RD unit uias diverted to a
200 gal reaction tank equipped with a mixer. A pH controller auto-
matically controlled the addition of a 1 percent slurry of lime to
maintain a pH between 7.4 and 7.8 in the reaction chamber- Neutral-
ized product water mas then pumped through a 10 micron cartridge
filter.
Table 30 shows the effectiveness of product neutralization.
Table 30. CHEMISTRY ANALYSES FOR RO PRODUCT NEUTRALIZATION
Acid-
Uater pH Alk. Cond. ity Ca Mg Fe Al SO,
Product 3.7
Neutral
product 7.4
0
5
55
27
9.3
0
0.37 0.20 0.25 0.19 0.33
5.1 0.20 0.04 0.10 0.40
All units expressed as mg/1 except conductance (Mmhos/cm) and pH.
An increase in calcium was expected since lime [Ca(OH) J uias
used as the neutralizing agent. With the decrease in iron and acid-
ity, the neutralized product was of potable quality.
Continuous RO product neutralization required (9.83 gram/m )
0.082 pounds of lime per 1,000 gal.
Discussion erf Norton Study
Fouling, which was observed during this long-term study, was severe
toward the end of the run. The fouling mechanism uas diagnosed as a
combination of organic and colloidal deposition and ferric hydroxide
precipitation. Several flushing techniques were successful in short-
term flux restoration, but rapid degradation recurred after each
flush.
The apparent reason for the fouling uas operation of the spiral
system at insufficient brine flou rates thus allowing boundary layer
81
-------
precipitation. This conclusion uas confirmed by superior flux sta-
bility of tube 3 as compared to tubes 1 and 2. Tube 3 performance
normally ujould be inferior since it uas subject to the most severe
concentration of pollutants. In this study, however, the superiority
of tube 3 uas attributed to a brine/product flow ratio which uas up
to 2.^ times the b/p ratio in tubes 1 and 2.
Injection of copper sulfate into the RO feed water determined
that the membrane uould reject copper at a 99.5 percent rejection
rate.
RD product water uas not of potable quality due to iron and pH.
Lime neutralization of the product uater resulted in a potable qual-
ity effluent.
Further testing uas necessary at higher brine/product flow ratios
to provide more representative long-term flux trends. Additional
tests along this line were made after the <* h unit returned from
Mocanaqua in Fall 1971.
MQCAIMAQUA FERROUS IRON STUDIES COMPARING SPIRAL-UOUND, HOLLQLJ-FIBER,
AIMD TUBULAR UNITS (15,16)
To investigate the Mocanaqua fouling phenomena, EPA and the
Commonuealth of Pennsylvania contracted uith Rex Chainbelt in 1971
to evaluate the iron fouling problem in the laboratory, to modify
the 1969 tubular system, and to conduct additional studies at
Mocanaqua. In order to make these studies more comprehensive, EPA
was to conduct simultaneous studies uith the k K spiral-uound RD
unit at the same site. A hollou-fiber RO permeator uas also
obtained for this study, and EPA later enlarged it to a three perm-
eator array for a hollou-fiber system of comparable size to the
spiral-uound system.
For the ensuing study, all three systems operated side by side
on the same uater; the only exception uas the acid injection to the
feed during the last phase of spiral-uound testing. Thus, a unique
opportunity uas provided for direct comparison of systems and for
investigation of the Mocanaqua iron fouling phenomenon.
82
-------
Typical uater quality characteristics of the Mocanaqua discharge
are presented in Table 31.
Table 31. TYPICAL RAU UATER QUALITY CHARACTERISTICS
DP MOCAWAQUA DISHCARGE
Parameter
pH
Conductance
Acidity
Calcium
Magnesium
Total iron
Ferrous iron
Aluminum
Sulfate
Manganese
Silica
TDS
Dissolved uxygen
Temperature
Units
Mmhos/cm
mg/1 as CaCO-,
mg/1
ii
n
M
n
ii
n
ti
n
n
°Fahrenheit
Value
3.<+
1100
230
120
90
80
68
11
800
15
10
1200
1
5k
The Rex Chainbelt Laboratory, in addition to the normal EPA
determinations, analyzed for silica by atomic absorption. A Hach
Kit uas used by Rex Chainbelt for on-site determinations of calcium,
total hardness, total iron, ferrous iron, and sulfates. A Myron L
TDS meter uas used for total dissolved solids measurements.
As a prelude to actual field investigations, laboratory studies
were performed by Rex Chainbelt to attempt to isolate possible causes
for the severe iron fouling seen at Mocanaqua during their 1969 tests.
From the results of these batch tests, Mason postulated that the
most probable cause of the observed fouling uas bacterial oxidation
of ferrous iron at the membrane surface and subsequent precipitation
of the resulting ferric iron uhich had been hydrolyzed.
For this reason, ultraviolet (UU) disinfection lights uere in-
stalled as part of the pretreatment system for all three field units
tested in the belief that the U\J light would kill most of the iron
oxidizing bacteria and thus inhibit or prevent bacterial oxidation
9 3
of Fe to Fe .
83
-------
Iron oxidation studies ujere performed during the actual field
study to evaluate the effectiveness of the UV light. Sixteen sets
of samples uere taken for one of these tests. Twelve of the 16
were raw feed samples that had passed through ID micron filters.
The remaining four sets were blended feed samples from the spiral
RD unit. Each individual set of samples consisted of five dupli-
cates. Ferrous iron was determined once per day on each set of
samples for a period of five days. To prevent contamination from
the pH probes and stirrers which uere used to determine ferrous
concentrations, only one of the duplicates was analyzed per day.
Following analysis, the sample uias considered contaminated and was
discarded.
All samples uere kept in a mine discharge at a 11°C (53°-54°F)
temperature to eliminate environmental changes. Those samples to
be kept dark uere placed in opaque plastic bags, placed in the
creek, and covered with brush to provide shade. Sulfuric acid uas
added to those samples in which the pH was lowered. Formaldehyde
uas used for a disinfectant uhere required. The results of the
test are given in Table 32. Specific conclusions relative to passi-
ble oxidation control techniques from the oxidation study were:
• ultraviolet disinfection inhibited oxidation;
• lowering the pH to 2.5 inhibited oxidation;
« some oxidation occurred in blended feed samples which
had been exposed to UU and kept in dark;
• at creek temperature (5k° F), virtually no oxidation
took place in 2k hours; and
• the oxidation mechanism uas bacteria since the above
variations in treatment inhibited oxidation.
Since some oxidation occurred in two of the blended feed samples
that had been exposed to ultraviolet treatment, it uas probable that
the U\7 did not effect a 100 percent kill. If bacteria were present
in the blended feed, it uas assumed that significant growth uas
probable at the membrane surface in the RO units.
-------
Table 32. FERROUS IRON OXIDATION CONTROL STUDY, MOCANAQUA, PA.
CD
LD
Ferrous concentration after:
Sample
Number
1
2
3
k
5
6
7
8
9
10
11
12
13
1<*
15
16
Note:
(a)n-n
2k
Initial hours
56
56
56
56
56
56
56
56
56
56
56
56
118
118
118
118
Results
56
56
56
56
56
56
56
56
56
56
56
118
112
118
118
expressed as
hours
56
56
56
56
56
56
56
39
56
39
56
118
112
112
118
mg/1.
72
hours
56
22
56
56
56
56
56
56
28
56
56
118
79
96
118
-.,-, fi 1 •*.„,
96
hours
56
1.8
56
56
56
56
56
56
28
56
28
56
118
39
96
118
Description(a'c)
Raw feed - light
Raid fpprl — rlark
Rau, ultraviolet-light
Rau, ultraviolet-dark
Raw, pH 2.5 - light
Raw, pH 2.5 - dark
Rau, UU, pH 2.5 - light
Raw, UU, pH 2.5 - dark
Raw, UU, disinfecttb; - light
Rau, UU, disinfect(b) - dark
Raw, disinfectib; - light
Rau, disinfect - dark
Blended feed, UU - light
Blended feed, UU - dark
Blended, disinfectCb\ UU -
Blended, disinfect(b), UU -
light
dark
\ ^Disinfection consisted of addition of 2 ml of formaldehyde to <*00 ml/sample.
All temperatures 53-5**°F except for initial blended feed sample temperature of 6**° F.
-------
Another series of oxidation tests at air temperatures 15.6° to
23.9° C (68-75° F) resulted in significantly faster oxidation rates
as is typical in most biological growth.
TUJO sets of spiral-wound modules were used in the 4 K unit
2
during the study. During Phase I, each module contained 4.65 m
(50 ft2) of standard percholate-modified cellulose acetate membrane
2 2
for a total unit membrane area of 41.9 m (450 ft ). The modules
2 2
used for Phase II contained 5.77 m (62 ft ) of Formamid-modified
2 2
cellulose acetate for a total unit membrane area of 51.9 m (558 ft ).
Figure 17 presents the system arrangement and flow diagram for
the spiral unit. Acid mine water was pumped through ten micron car-
tridge filters and a LJU disinfection light before entering the re.-
vsrse osmosis unit. UW disinfection was believed necessary to
inhibit bacteriological oxidation of the ferrous iron uhich had
ii
presumably contributed to fouling observed in earlier studies.
During Phase II, sulfuric acid was injected to lower the blended
feed pH to 2.9 and thus inhibit both ferrous oxidatidn and ferric
precipitation.
The second unit tested was a hollow-fiber system, manufactured
by DuPont; initially, it consisted of one permeator on loan from
DuPont to Rex Chainbelt. As illustrated in Figure 3, approximately
2 2
139.6 m (1500 ft ) of B-9 hollou-fiber nylon membrane were packed
in a 15.2 cm x 1.22 m (6 in x 4 ft) stainless steel pressure vessel.
During Phase I, the single DuPont permeator operated at 2758 k(\l/m2
(400 psi) from a Moyno high pressure pump which also supplied feed
water to the tubular unit. Phase I DuPont tests were successful
so EPA purchased two additional permeators for Phase II and formed
a three permeator array, 6 K unit, as shown in Figure 18. The brine
from both new psrmeators in parallel served as the feed to permeator
number 3 (the original Phase I permeator). Flow control orifices
were placed in each brine line from permeators 1 and 2 to ensure
equal brine flows and prevent system unbalance. Because high brine
flows are not required for hollow fiber systems, it was not necessary
86
-------
CD
-O
Blended
Raw
Feed
Feed
Tube 1
Tube 2
Tube 3
Recycled Brine
1892
Liter
Supply
Tank
High Pressure
Pump
Deep Mine Portal
r—I.jn (50° sal)
j Acid J
(Injection)
I I
Product Water
Waste
Brine
Figure 17. Spiral -wound reverse osmosis system arrangement at Mocanaqua, Pa.
-------
Raw Feed
33
03
Module 1
Flow Control
Orifice
Module2
Module 3
Brine
Product Water
Ultra-
Violet
Light
High Pressure Pump
Deep Mine Portal
Figure 18. Hollow-fiber reverse osmosis system
arrangement at Mocanaqua, Pa.
-------
to recycle brine. Therefore, the unit received raw acid mine water
that had been filtered and had passed through the ultraviolet light
for disinfection.
Phase I tubular studies ' utilized a unit consisting of sixty
7.6 cm x 2.39 m (3 in x 7 ft ID in) plastic tubular #310 modules
illustrated in Figure 19 and arranged as shown in Figure 20. The
tubular system was manufactured by Calgon-Havens Company. Each
module contained eighteen 1/2 in (1.27 cm) i.d. porous fiberglass
tubes that were lined with cellulose acetate membrane and connected
2 2
in series. Membrane area was 1.57 m (16.9 ft ) per module for a
2 2
total system membrane area of Vk.k m (101^ ft ). Pretreatment was
the same as that for Phase I Gulf and DuPont, i.e., 10 micron fil-
tration and UU disinfection.
Turbulence promotion rods were placed in modules where brine
flow was lowest to inhibit 'boundary layer1 precipitation and fouling.
Unfortunately, use of turbulence promoters also resulted in high
pressure drops across the modules in which they were installed, thus
reducing the average applied pressure.
During Phase II, the sixty #310 modules were replaced with five
2 2
#610 modules for a total membrane area of 7.87 m (8*4.5 ft ).
It was necessary to determine the osmotic pressure of the water
in order to compensate for variations in water quality and recovery,
Ik
The spiral-wound unit was modified to enable measurement of osmotic
pressure by pressure differences between the brine and product side
of the membrane. By varying recovery, osmotic pressure measurements
were made over a complete range of concentrations and a correlation
was developed between brine conductivity and osmotic pressure.
Since acid injection was utilized in Phase II spiral-wound studies
and since acid affects conductivity, a different correlation was
necessary for Phase II. Both equations and plots are shown in
Figure 21.
89
-------
SINGLE TUBE WITH TURBULENCE PROMOTER ROD
TURBULENCE
PROMOTER
ROD END VIEW
18 POROUS
FIBER GLASS TUBES
IN SERIES
PRODUCT
WATER SHROUD
FEED WATER
MODULE ASSEMBLY
PRODUCT WATER
Figure 19
Tubular reverse osmosis module configuration' ' at Mocanaqua, Pa
-------
Raw Feed
,\\
H I
H 1
i i i
h
i
i i i h
-n i i i \\-
-D
l l I
-T
H
n_
_
1 1 I
1 1 1
1
Ih
H
L
EachQ represents one module as shown in Figure 19
r| 1
^ i
-i 1 1
M 1 1
\.
*" \Filter / —
Ultra
1 Ink*
Wh
1
lV|Yl|-
1
|V|VH-
I
|v VJ|J
1
H 1 IVIY
EH
H 1 IYIYIY
»• H
igh Pressure Pump
••!•••
l| Waste Brine
J
Product Water
1
H8>-J
60 modules @ 1.57m* (16.9 ft* ) membrane each 3 banks,
5 modules in series, each row modules marked with a V have
volume displacement (turbulence promoter) rods
Deep Mine
Portal
Figure 20* Phase I module arrangement
study at Mocanaqua, Pa.
06)
for tubular reverse osmosis
-------
- 200
- 150
in
a.
VD
U)
4)
O
E
Ifl
O
No Acid
Injection
100
v)
VI
4)
ito
a.
u
«•
O
E
v>
O
1000 2000 3000 4000
Conductivity (C) micromhos/cm
Figure 21
Osmotic pressure - conductivity relationships at Mocanaqua, Pa.
-------
Spiral-Wound Phase I Studies
Phase I of the spiral-wound studies was made at a unit recovery
O
of 75 percent and system operating pressure of 4138 kl\l/m (600 psi).
A summary of operating parameters for this study is given in Table 33.
Water temperatures of 63° F were caused by the Gould high-pressure
pump that imparted energy to the 54" F ram AMD. The necessity of
brine recycle only aggravated the temperature rise since a portion
of the uater was continually recycled through the pumps. The in-
creased temperature benefitted observable flux rates since product
flDu uas strongly temperature dependent. Since all data were cor-
rected for temperature, the higher operating temperature uas not
a factor in data evaluation. In actual operation, however, the
V
higher the temperature, the higher the flux. Overall system recov-
ery during Phase I uas maintained at 75 percent during the first
1,054 hr of operation. The log-log flux decline slope uas -0.034
for tube 1 and -0.032 for tube 3 during this period. At 1,054 hr
elapsed time, the ultraviolet light uas turned off to determine its
effectiveness in controlling flux decline. As shown in Figure 22
(linear plot) and Figure 23 (log-log plot), the increase in flux
decline was dramatic with the log-log slope increasing to near
-0.2 even though recovery remained at 75 percent. Following a
phosphoric acid flush, the U\J uas turned on again but recovery uas
increased to 84 percent. Flux decline uas so severe at 84 percent
recovery (log-log slope greater than -4.0) that the run was termin-
ated after only 70 hours at that recovery level and flushed again
uith phosphoric acid. Though the acid flush improved flux, it did
not stabilize on the original slope, presumably indicating all the
fouling had not been removed. Total operating time during Phase I
was 1,922 hr.
Fouling observed at 84 percent recovery was attributed to cal-
cium sulfate precipitation. Analysis of the acid flush water con-
firmed the presence of large amounts of both iron and calcium after
the 84 percent recovery run. A loss of calcium, sulfate, and iron
93
-------
Table 33. OPERATING PARAMETERS FOR SPIRAL-WOUND PHASE I STUDY AT
75 PERCENT RECOVERY AT MOCANAQUA, PENNSYLVANIA
Parameter Value
Raw water feed flow, gpm 6.02
Product water flow, gpm 4.50
Brine water discharged, gpm 1.52
Brine water recycled, gpm 4.26
Minimum brine/product flow ratio (Tubes 1 and 2),
ratio/module 5:1
Maximum brine/product flow ratio (Tube 3),
ratj.o/module 12:1
Water recovery, percent 74.8
Recovery of blended feed, percent 43.8
Feed pressure, psig 602
Feed water temperature, °F 62.6
Tube one flux, gal/ft2/day @ 600 psi net and 77° F 19.56
Tube two flux, gal/ft2/day @ 600 psi net and 77° F 19.52
Tube three flux, gal/ft2/day @ 600 psi net and 77° F 18.77
Length of run, hours 1672
Date of run May 1 - July 12, 1971
All values are means from 73 data sets.
Note: To convert flux (gal/ft2/day @ 600 psi and 77°F) to liters/
m /day 8 4138 kN/m2 and 25°C, multiply by 40.67; to convert gallons
per minute to liters/second, multiply by 0.063; and to convert psi
to kN/m2, divide by 0.145.
-------
85% Recovery
Ul
O Tube 1
• Tube 3
o
ui
CN
TJ
C
O
CM
1200
1000
00
CO
o
TJ
CN
800
600
4-
4-
1-
300
600
900
1200
1500
1800
2100
ELAPSED OPERATING TIME, hours
Figure 22
Phase I spiral-wound reverse osmosis unit flux rates at
Mocanaqua, Pa.
-------
UD
cn
a
TJ
o
c
-o
c
a
o
30
20
O
O)
at
X
10
8
7
6
5
4
3
Note: Recovery 75% Except Where Noted
Spiral Wound RO
Unit Phase I
Tube 3
Tube 1
Spiral Wound RO Unit Phase II 400PSI
Tube3
Q/
00
Slope-0.01
Hollow Fiber RO Unit
Phase II 400 PSt
o>
Note: Module 3 Total Elapsed Time is +838 Mrs
From Phase I
1 gal/f ft2/day=40.7 Iiter/m2/day
77°F = 25°C 600 psi= 4138 kN/m2 400 psi- 2759 kN/m 2
I I I I I I I I
10
20 30 50 100 200
ELAPSED TIME, hours
Figure23
500
1000
2000
A summary of reverse osmosis flux trends at Mocanaqua, Pa.
-------
was detected in the routine chemical analyses as noted in Table 35.
At 75 percent recovery and the U\J off, it was felt that bacterial-
propogated iron precipitation uas causing the flux decline.
Operating parameters for the spiral-wound unit during the 84
percent recovery run are given in Table 34.
Chemical analyses for the 75 percent recovery operation (Table
35) indicate a 99+ percent rejection on all multivalent ions. Prod-
uct waters would still require treatment for iron and manganese and
pH adjustment before potable water quality criteria could be met.
Spiral-Mound Phase II Studies
The manufacturer suggested that increasing the b/p flow ratio
would decrease the log-log slope observed during Phase I. One way
of accomplishing a b/p increase was to lower the operating pressure
and thereby reduce product flow. Lowering input pressure to
2
2758 kIM/m (400 psi) would also serve to lessen membrane compaction
which contributes to flux losses. During Phase I, the maximum b/p
ratio per module was 12:1 and the minimum was 5:1 (from Table 33).
During Phase II, the maximum b/p ratio was 22:1 and the minimum
10:1 (Table 36) which amounted to about a 200 percent increase over
Phase I.
As the earlier oxidation tests had shown pH control to be an
effective oxidation inhibitor and as the lower pH would also inhibit
precipitation of the ferric iron already present, sulfuric acid was
injected into the feed water to lower the blended feed pH to 2.9.
The UV light was also used during the majority of this Phase II
study.
Table 36 presents the operating parameters for this 2,454 hr
Phase II study at 75 percent recovery.
Early in the study, leaks were observed in tubes 1 and 2. By
probing each module and measuring the conductivity of product water
at various points along the inside of the modules' product tubes,
97
-------
Table 34. OPERATING PARAMETERS FOR SPIRAL-WOUND PHASE I STUDY AT
84 PERCENT RECOVERY AT MOCANAQUA, PENNSYLVANIA
Parameter
Raw water feed flow, gpm
Product water flow, gpm
Brine water discharged, gpm
Brine water recycled, gpm
Minimum brine/product flow ratio (Tubes 1 & 2),
Value
4.92
4.13
0.79
5.50
ratio/module 8:1
Maximum brine/product flaw ratio (Tube 3),
ratio/module 12:1
Water recovery, percent 83.9
Recovery of blended feed, percent 39.6
Feed pressure, psig 600.0
Feed water temperature, °F 66.6
Tube one flux, gal/ft2/day S 600 psi net and 77°F 17.03
2
Tube two flux, gal/ft /day @ 600 psi net and 77°F 17.06
Tube three flux, gal/ft2/day @ 600 psi net and 77°F 16.25
Length of run, hours 70
Date of run July 13 - July 17, 1971
All values are means from four data sets.
Note: To convert flux (gal/ft2/day @ 600 psi and 77°F) to liters/
2 2
m /day @ 4138 kN/m and 25°F, multiply by 40.67; to convert gallons
per minute to liters/second, multiply by 0.063; and to convert psi
to kN/m2, divide by 0.145.
98
-------
Table 35. CHEMICAL ANALYSES FOR SPIRAL-WOUND STUDIES AT MOCANAQUA, PENNSYLVANIA
Sample
Designation
pH
Cond.
Acid-
ity
Cal-
cium
Spiral-mound
Rau feed
Blended feed
Brine
Product x ,.
Rejections a
3.4
3.1
2.9
4.4
1080
2070
3540
17
99.2%
240
460
810
38
91.7%
130
260
490
0.4
99.8%
Spiral-wound
Raw feed
Blended feed
Brine(b)
Brine
Product
3.4
3.0
2.9
4.4
1010
2800
4800
23
210
700
(1260)
1290
10
180
400
(1080)
760
0.7
Spiral-wound
Rau feed
Acidified feed
Blended feed
Brine
Total product
Overall re-
jections'8)
Tube 1
Rejections'8^
Tube 3
Rejections^8)
3.4
2.9
2.8
2.7
3.8
1110
1520
2830
4150
67
97.6%
86
97.0%
37
98.7%
220
420
610
880
33
94.6%
_
140
140
330
520
1.3
99.6%
1.6
99.5%
0.55
99.8%
Magne-
sium
Total
iron
Phase I @ 75 Percent
88
170
310
0.3
99.8%
77
180
330
0.4
99.8%
Phase I @ 85 Percent
130
380
(780)
710
0.8
Phase II @
110
110
260
380
4.0
98.5%
3.1
98.8%
0.75
99.7%
140
310
(840)
540
0.5
Ferrous
iron
Alum-
inum
Sul-
fate
Man- Dissolved
qanese oxyqen
Recovery
64
130
250
0.3
99.8%
12
24
44
0.2
99.2%
750
1340
2300
0.9
99.9%
- < 1.0
<1.0
<1.0
Recovery
78
250
(470)
440
0.35
15
55
(90)
100
0.5
850
1420
(5100)
2840
1.0
75 Percent Recovery
100
100
250
370
2.4
99.0%
3.3
98.7%
0.68
99.7%
73
77
190
280
2.0
98.9%
_
-
_
14
14
33
54
0.8
97.6%
1.1
96.7%
0.75
97.7%
930
980
2110
3130
19
99.1%
30
98.6%
5.8
99.7%
17
17
43
68
0.5
98.8%
0.6
98.6%
0.21
99.5%
^Rejections = (blended feed - product)/blended feed X 100.
Brine values in parenthesis mere calculated based on the recovery of the reverse osmosis unit and assuming
the raw feed values mere correct. At 83.4 percent recovery, the concentration factor is 6.02. This calcu-
lation was necessary since massive precipitation occurred in the brine sample before analysis could be made
at Norton.
Note: All units are mg/1 except pH and specific conductance (micromhos/cm).
-------
Table 36. OPERATING PARAMETERS FOR SPIRAL-WOUND PHASE II STUDY AT
75 PERCENT RECOVERY AT MOCANAQUA, PENNSYLVANIA
Parameter ___________ Value
Rau water feed flow, gpm 5.IB
Product water flow, gpm 3.86
Brine water discharged, gpm 1.32
Brine water recycled, gpm 6.32
Minimum brine/product flow ratio (Tubes 1 & 2),
ratio/module 10:1
Maximum brine/product flow ratio (Tube 3), ratio/module 22:1
Water recovery, percent 74.5
Recovery of blended feed, percent 33.6
Feed pressure, psig 399
Feed water temperature, °F 66.6
Tube one flux, gal/ft2/day @ 400 psi net and 77°F 12.81
Tube thio flux, gal/ft2/day § 400 psi net and 77°F 12.55
Tube three flux, gal/ft2/day @ 400 pai net and 77°F 11.58
Length of run, hours 2,454
Date of run July 27 - November 9, 1971
All values are means from 100 data sets.
Note: To convert flux (gal/ft2/day @ 400 psi and 77°F) to liters/
2 2
m /day @ 2758 kN/m and 25°C, multiply by 40.67; to convert gallons
per minute to liters/second, multiply by 0.063; and to convert psi
to kN/m2, divide by 0.145.
100
-------
all leaks were found to be near the ends of the modules where glue
connected the membrane to the perforated product tube (see Figure 1).
The modules weren't replaced because considerable operating time
would be lost and since modules in tube 3 had no leaks, their product
quality would be representative of normal modules. Also, as the
leaks in tube 1 and 2 were very small, they would have no effect on
flux studies. Therefore, chemistry data in Table 35 are given for
product water from tubes 1 and 3 as well as for the entire unit.
Although unit rejections were lower for Phase II than for Phase
I because of the leaks, tube 3 rejections were comparable to Phase
I results.
A log-log plot of Phase II flux is given in Figure 23. Log-log
slopes of -0.012 for tube 1 and -0.009 for tube 3 were obtained
during the 2,^5^ hr of operation at 75 percent recovery. These
values were improvements over the -0.03^ slopes from Phase I. The
combination of acid injection to inhibit precipitation of ferric
hydroxide and the higher b/p ratios and brine flow rates were be-
lieved responsible for the flux stabili?ation. Discontinuing use
of the ultraviolet light at 2,002.5 hr elapsed time had no apparent
effect on flux stability.
Possibly the higher b/p ratio and correspondingly higher brine
flow rates—or acid injection alone—may have been solely responsible
for flux improvement, but unfortunately, no tests were made to prove
or disprove this conjecture.
A phosphoric acid flush at the end of the 2,^54 hr study did
not improve flux.
Approximately 60 ml of sulfuric acid (98 percent, technical
grade) was required to treat each 1,000 gal of water entering the
RO unit in order to lower blended feed pH to 2.9. This amounted to
27 mg of concentrated acid per liter of water treated.
101
-------
Hollow-Fiber Phase I Studies
Phase I hollow-fiber testing began with a single permeatar
2
operating at 75 percent recovery at 2758 k!\!/m (400 psi) and con-
tinued for a total of 838 hr- Operating parameters are given in
Table 37 and chemical data are presented in Table 40.
Rejections of all multivalent ions were in the range of 99 per-
cent based on raw feed. These rejections, though slightly less than
the spiral-ujound, uere still excellent. As ujith the spiral unit,
the product water would require treatment for pH, iron, and manganese
before potable standards could be met.
The flux trend for the single hollow-fiber permeator is shown
linearly in Figure 24 and on a log-log basis in Figure 25. The log-
log flux decline slope was O.D37 during the 838 hr study. This flux
decline slope was comparable to Phase I spiral-wound results. A
small increase in pressure drop across the permeator was observed
which probably indicated minor iron fouling.
PhaseII Hollow-Fiber Studies
For Phase II studies, two additional permeators were added to
the Phase I system to form a 2-1 array as shown in Figure 17. The
Phase I permeator, which had accumulated 838 hr of operation, was
used as the last permeator in the array. The permeators were opera-
ted in this 2-1 array to allow high recovery experiments and confine
the expected calcium sulfate fouling to a single permeator. Gener-
ally, hollou)-fiber units are not used in staged arrays but are
arrayed for parallel operation since brine flow requirements for
hollow-fiber systems are not as critical as for tubular and spiral-
wound systems.
During Phase II, several variations in operating parameters were
made. In order to evaluate the effect of the ultraviolet light on
system operation, the light was turned off from 140 hr elapsed time
(e.t.) through 595 hr e.t. This time interval represented 978-1433
hr e.t. on permeator number 3 (last stage permeator). As seen in
102
-------
Table 37. OPERATING PARAMETERS FOR HOLLOW-FIBER PHASE I STUDY AT
75 PERCENT RECOVERY AT MOCANAQUA, PENNSYLVANIA
Parameter
Raid water feed flow, gpm
Product mater flow, gpm
Brine water discharged, gpm
lijater recovery, percent
Feed pressure, psig
Feed water temperature, °F
Unit flux, gal/ft2/day @ 77°F and 400 psi net
Value
2.08
1.55
0.53
7k. 4
400.0
53.3
2.32
Length of run, hours 638
All values are means from 78 data sets.
Note: To convert flux (gal/ft2/day @ 400 psi and 77°F) to liters/
m2/day @ 2758 kN/m2 and 25°C, multiply by 40.67; to convert gallons
per minute to liters/second, multiply by 0.063; and to convert psi
to kN/m2, divide by 0.145.
103
-------
00
O
-o
c
o
o
o
E
Q.
O>
t—
u
13
Q
O
of
0.
2.25 -
2.0 -
1.75 —
Operated as a Single Permeator
Water Recovery - 74.3 ± 0.28%
I— Brine Flow - 0.54 ±. 0.01 gpm
0.14
200
400
600
800
2.0
1.75
1.5
Operated as Final Stage
Permeator in a 2-1 Array
I Overall Water Recovery
Percent
I
I
0.12
0.11
0.10
0.09
I
II
III
IV
76.2 ± 0.6
84.4 ± 0.7
78.5± 0.5
75.3 ± 0.5
800 1200 1600 2000 2400
ELAPSED TIME, hours
2800
Figure 24
Operational history of hollow-fiber permeator #691
during the Mocanaqua study
o
CN
-o
C
o
CN
E
10
K
CN
u
D
a
O
Qi
a.
-------
a
ui
I III
Tubular RO Unit Phase 2 600 PSI
Slope-0.04
Slope-0.037
Note:l gal/ft2/day=40.7 Iiter/m2/day
77°F = 25°C Hollow Fiber Permeator
,si = 4138kN/m2 #691(400PSI)
I
See Figure 24 for
Details of Run
I I
10
20
40 70 100 200 400
ELAPSED TIME, hours
700 1000
2000 3000
Figu re 2 5
Tubular and hollow-fiber reverse osmosis unit flux
trends during the Mocanaqua study.
-------
Figure 23, no apparent flux trend change occurred as a result of no
UU. This was opposite to the dramatic slope change which occurred
on spiral-uound Linen the UU was turned off.
At 390 hr through 426 hr, e.t., the system recovery was increased
to 85 percent. This increase in system recovery had very little
effect on the recoveries of permeators 1 and 2 whose recoveries were
still below 65 percent. Thus, very little change in flux occurred
in the first two permeators during this high system recovery opera-
tion. Permeator 3, however, which was subject to the most severe
pollutant concentrations, suffered a drastic flux loss. Upon lowering
recovery again to 75 percent, permeator 3's flux again stabilized
(Figure 23).
At 596 hr elapsed time (1,434 for permeator 3), the UU light was
turned on again but system recovery was increased to 85 percent.
These operating conditions were maintained for 111 hr, including
operating at SO percent recovery for 38 hr, before system recovery
was lowered (707 hr e.t., 1,545 e.t. for permeator number 3).
Again, severe flux losses occurred in permeator 3 (log-log slope
= -1.77). Although the flux in permeator 3 stabilized, it was now
following a significantly steeper flux decline slope (log-log slope =
-0.36 at 78-80 percent recovery). A subsequent flush with disinfect-
ant failed to improve flux. Sodium hydrosulfide was used to flush
permeator 3 at 2,081 hr (on permeator 3) and successfully restored
flux to the original flux decline slope of -0.037 at 78 percent re-
covery. Flux immediately dropped again, however, but stabilized at
lower values until the end of the run at 2,670 hr e.t. (permeator 3).
Permeators 1 and 2 appeared to suffer a flux slope change near
600 hr elapsed time after following an initial slope of -0.015 until
that time. Following the 85 percent recovery test which ended at
707 hr elapsed time, first stage permeator flux stabilized following
a log-log slope of -0.03 for approximately 540 hours until 1,243 hr
e.t. During the last 590 hr of operation, all three permeators lost
106
-------
and then regained flux prior to a final sodium hydrosulfide flush.
This flush virtually restored first stage permeator flux to the
original -D.015 slope values. Since the test uas terminated at
this point, it uas not possible to determine if the -O.D15 slope
could be maintained following the flush. Although the flush im-
proved permeator 3's flux, it did not return the flux to the orig-
inal slope values.
A post mortem analysis of permeator number 3 by the manufacturer
revealed that the fouling uas largely due, as expected, to calcium
sulfate precipitation.
In the case of the tuo first stage permeators uhose flux had
2
been restored by the final flush, an additional 214 kIM/m (31 psi)
pressure drop had been acquired during the study uhich uas not
removed. Since neither of these first stage permeators had ever
operated above 66 percent recovery, it must be assumed that iron
fouling caused the flux losses and pressure drop increase as it is
unlikely that calcium sulfate uould precipitate at that recovery
level on the Mocanaqua uater.
Operating parameters for Phase II hollou fiber at 75 and 85
percent recovery are given in Tables 38 and 39 respectively. Chemi-
cal data from 75 percent recovery operations are reported in Table k
Rejections during Phase II uere comparable to Phase I results,
i.e., in the range of 99 percent based on rau feed.
A complete log-log flux plot for the initial permeator, uihich
uas used both in Phase I and Phase II, is given in Figure 25. This
permeator operated for 2,670 hr (838 during Phase I and 1,832 during
Phase II).
Significant variations uere noted in the log-log flux curve of
the hollou-fiber unit. The slope appeared to increase as brine
flou decreased and a possible relationship may exist in the form of
a b/p flou limit although insufficient data uere available to sub-
stantiate this relationship. As brine flou rates decreased, recov-
ery and risk of precipitation increased and this may have caused
107
-------
Table 38. OPERATING PARAMETERS FOR HOLLOW-FIBER PHASE II STUDY AT
75 PERCENT RECOVERY AT MOCANAQUA, PENNSYLVANIA
Parameter
Value
Raui water feed flow, gpm
Total product flow, gpm
Brine water discharged, gpm
Unit ttiater recovery, percent
Feed pressure, psig
Feed temperature, °F
Permeatar No. 1 product flaw, gpm
Recovery, permeator No. 1, percent
2
Flux, permeator No. 1, gal/ft /day
Permeator No. 2 product flow, gpm
Recovery, permeator No. 2, percent
Flux, permeator No. 2, gal/ft2/day @ 400 psi & 77°F
Permeator No. 3 product flow, gpin
Recovery, permeator No. 3, percent
2
Flux, permeator No. 3, gal/ft /day
Length of run, hours
Date of run
6.18
4.?2
1.46
76.4
400
54.3
1.86
59.9
2.78
1.83
59.5
2.74
1.03
41.4
400 psi net & 77°F 1.92
1667
June 10 - August 28, 1971
400 psi net & 77°F
All values are means from 83 data sets.
Note: To convert flux (gal/ft2/day @ 400 psi and 77°F) to liters/
m2/day @ 2758 kN/m2 and 25°C, multiply by 40.67; to convert gallons
per minute to liters/second, multiply by 0.063; and to convert psi
to kN/m2, divide by 0.145.
108
-------
Table 39. OPERATING PARAMETERS FDR HOLLOW-FIBER PHASE II STUDY AT
85 PERCENT RECOVERY AT MOCANAQUA, PENNSYLVANIA
Parameter Value
Raw water feed flow, gpm 5.73
Total product flow, gpm 4.86
Brine water discharged, gpm 0.87
Unit water recovery, percent 8k.8
Feed pressure, psig 400
Feed temperature, °F 54.0
Permeator No. 1 product flow, gpm 1.89
Recovery, permeator No. 1, percent 65.5
Flux, permeator No. 1, gal/ft/day @ ^00 psi net & 77°F 2.84
Permeator No. 2 product flow, gpm 1.85
Recovery, permeator No. 2, percent 65.0
Flux, permeator (Mo. 2, gal/ft2/day § <+00 psi net & 77°F 2.78
Permeator No. 3 product flow, gpm 1.12
Recovery, permeator No. 3, percent 56.3
Flux, permeator No. 3, gal/ft2/day @ ^00 psi net & 77°F 2.10
Total operating time @ 85 percent recovery, hours 147
Longest run, hours 111
Date of run 6/26-6/28/71, 7/5-7/9/71
All values are means for 11 data sets.
Note: To convert flux (gal/ft2/day @ <+DO psi and 77°F) to liters/
rj O
m /day @ 2758 kN/m and 25°C, multiply by 40.67; to convert gallons
per minute to liters/second, multiply by 0.063; and to convert psi
to kN/m2, divide by 0.145.
109
-------
Table 40. CHEMISTRY ANALYSES FOR HOLLOU-FIBER STUDIES AT MDCANAQUA, PENNSYLVANIA
Sample
Designation
(a)
Raw feedva'
Brine(a)
Product(a)
Rejections
Raw feed
Brine
P Product
Rejections(b)
All units are
a Analyses by
Rejections
pH
3.4
2.9
4.5
3.4
3.0
4.3
mg/1
Rex
= Raw
Acid-
Cond. ity
_ —
_ _
— _
_
1020 210
3400 720
32 32
96.9% 84.8%
Cal- Magne-
cium slum
Phase I @ 75
110 80
420 310
0.55 0.59
99.5% 99.3%
Phase II 6
150 115
590 410
1.2 1.4
99.2% 98.8%
Total Ferrous
iron
Percent
65
260
0.54
99.2%
iron
Recovery
59
230
0.52
99.1%
Alum-
inum
( I C 1 C •)
8.0
31
0.18
97.8%
Sul-
fate
740
2700
2.2
99.7%
TDS
1250
4900
28.
97.8%
Manga-
nese DO
14
53
0.08
99.4%
Sil-
ica
10
43
0.49
95.1%
1 75 Percent Recovery
110
440
1.2
98.9%
except for pH and specific conductance
Chainbelt. All
other analyses
by EPA.
71
300
0.76
98.9%
15
58
0.80
94.7%
940
3000
4.6
99.5%
1320(a)
5810(a)
2.5(a)
98.1%
14(a)<1.0(
57(a)<1.0(
0.12(a)<1.0(
99.1%
a) n
a) 49
a) 0.83
(a)
(a)
(a)
92.5%
(micromhos/cm) .
feed concentration-product concentration y inn
Raw feed concentration
-------
the observed slope changes. Whatever the reason, flux slopes were
minimized when the brine flow rate uas in excess of 3.785 1/min
(1 gal/min).
Tubular Unit15'16 Phase I Studies
The tubular RO system uas also operated in tujo separate phases
during this study. Phase I utilized 60 Type 310 modules in a
6-4-2 array with five modules in each series in each rou. The last
two modules in bank 2 and the last 3 modules in bank 3 contained
volume displacement rods (WDR) that increased the brine velocity.
The normal inside diameter in the tubular system is # in (1.27 cm)
ujhich corresponds to a linear brine velocity of 1.64 ft/sec per gpm
of brine flou (0.132 m/sec per liter/min). The volume displacement
rods effectively increased this velocity to 2.5 ft/sec per gpm
(D.2 m/sec per liter/min) of brine flou. When utilizing UDR's, head-
loss through the module increased significantly. In a module uithout
l/DR's, the' headless at one gpm (3.785 1/min) brine flou uas five psi
2
(34.5 kl\l/m ) per module, while with UDR's this increased to 22 psi
(151.7 kl\l/m2) per module.
2
Initial Phase I operation uas at 6DD psi (4138 k(\)/m ) and 75 per-
cent recovery. During Phase I, the product water flux decreased
steadily from 13 gal/ft2/day to 8.5 gal/ft2/day (345 l/m2/day) in
only 48D hours. It uas originally assumed that the system had been
contaminated uith iron oxidizing bacteria because of trouble experi-
enced with the LJW light. At 16D hr, the system uas disinfected uith
a quatenary ammonium compound (L-ll-X), and n slight increase in flux
uas noted. However, membrane relaxation probably occurred during
this time since the unit operated at lou pressure. Relaxation
generally results in a flux increase for a short period of time.
Immediately after the disinfection, the flux continued to decline
rapidly. flt this point, it uas felt that the brine velocities might
possibly be too lou and that concentration polarization effects uere
causing the rapid fouling. Minimum brine velocities uere increased
from 1.2 - 1.4 ft/sec to 2.0 - 2.2 ft/sec (0.37 m/s - 0.67 m/s).
Ill
-------
Phase I chemical data are presented in Table 41.
Tubular Unit Phase II Studies
At the end of Phase I, it uas noted that the flux declines ex-
perienced with the tubular system uere not experienced with the hollou-
fiber system or the spiral-uound system also operating alongside.
It uas also noted that both the spiral-uound system and the hollou-
fiber system had considerably louier salt passage (higher rejection)
as compared to the tubular system. The high salt passage of the
tubular 31D membrane may hav/e had some influence on the flux de-
clines experienced. To test this, five high-flux—louj-salt-passage
modules (type E61D) uere installed and put into operation for Phase
II. During Phase II, recovery uas limited to less than 50 percent
o
at 4138 kl\l/m (600 psi) due to the use of only five modules. Operat-
ing parameters for this 807 hr study are given in Table 42 and
chemical data are presented in Table 41. Rejections uere higher for
Phase II (type E610) membranes than for Phase I membranes (type 310).
Figure 25 presents the flux history for these modules. An extremely
high initial compaction uas experienced during the first feu hours
of operation. The flux then stabilized on a -0.040 log-log slope
for the first 300 hr. A gradual decline then occurred through
n
about 440 hr, at uhich time the flux stabilized at 13.7 gal/ft/day
9
(557 1/m /day) for the remainder of the study. The change in the
flux decline slope experienced from near 300 hours e.t. uas also
noticed to a lesser degree on the hollou-fiber unit and uas believed
caused by a higher-than-normal iron (III) content in the AMD. The
decline uas probably entirely due to iron fouling since operation
at 40-45 percent recovery uas uell belou the CaSO fouling range.
The modules uere flushed uith a sodium hydrosulfite solution (4 ut
percent) for 1 hr. This resulted in a dramatic increase in flux
as shoun in Figure 25. Since additional operating time uas not
available, it is not knoun hou much of this flux increase uas due
to cleaning and hou much uas due to membrane relaxation. It is
felt that a substantial gain uas accomplished since membrane relaxation
112
-------
Table 41. CHEMISTRY ANALYSES FOR TUBULAR STUDIES(15>16) AT MOCANAQUA, PENNSYLUANIA
Sample
Designation pH
Raui feed
Brine
Product
Rejections
3.4
3.1
4.2
Acid-
Cond. ity
1050 250
2400 560
46 46
95.6% 81.6%
Cal-
cium
125
330
2.2
98.2%
Magne-
sium
Phase I
92
240
1.4
98.5%
Phase II 8
Raw feed(a
Brine(a)
Product(a)
Rejections
> 3.4
3.1
4.3
—
Analyses by Rex
All other
All units
So i o r"fc i nnca
analyses
-
— —
Chainbelt.
by EPA.
110
200
0.6
99.5%
83
150
0.45
99.5%
Total
iron
Ferrous
iron
Alum- Sul- Manga-
inum fate TDS nese DO
Sil-
ica
@ 75 Percent Recovery
78
230
0.9
98.8%
61
150
1.0
98.4%
12 660 1320(a) 14(a)
30 1650 3520(a) 39(a)
1.0 4.4 53(a) 0.31(a) -
91.7% 99.3% 96.0% 97.8%
11
16
7.2
34.5%
1 42.5 Percent Recovery
70
130
0.4
99.4%
are mg/1 except for pH and specific conductance
Raw feed concentration-product concentration
63
160
0.62
99.0%
8.3 800 1320 14
15 1450 2300 25
0.15 2.0 25 0.08
98.2% 99.8% 99.6% 99.4%
12
21
1.0
91.7%
(micromnos/cm ) .
x inn-
Raw feed concentration
-------
Table 42. OPERATING PARAMETERS FOR TUBULAR PHASE II STUDY AT 43
PERCENT RECOl/ERY<15,16) AT MOCANAQUA, PENNSYLVANIA
Parameter Value
Raw water feed flow, gpm 1.48
Product water flow, gpm 0.63
Brine water discharged, gpm 0.65
Water recovery, percent 42.5
Feed pressure, psig 617.0
Feed water temperature, °F 55.0
Unit flux, gal/ft2/day 8 77°F & 600 psi net 15.60
Length of run, hours 807
All values are means from 34 data sets.
Note: To convert flux (gal/ft2/day @ 600 psi and 77°F) to liters/
m2/day 9 4138 kN/ro2 and 25°C, multiply by 40.67; to convert gallons
per minute to liters/second, multiply by 0.063; and to convert psi
to kN/m2, divide by 0.1,45.
114
-------
alone would not account for an increase in flux of about 33 per-
cent.
The salt passage properties for both the types 310 and 610
tubular modules are shown in Table 43. The salt passage uas cal-
culated based on average brine concentration experienced on the
membrane, i.e., the average of feed and brine concentrations.
This procedure allows comparison of salt passages while operating
the RO system at different product water recoveries.
Generally, salt passage for the type 310 modules ranged from 1
to 1.5 percent for Ca, Mn, Fe, Al, and SO,. Silica passage was
extremely high at an average percent of 54. The type 610 modules
had significantly lower salt passage; i.e., 0.4 to 0.5 percent for
Ca, Mg, Mn, Fe, Al, and SO.. Silica passage was also considerably
lower than the 310 modules at an average percent of 6.2 percent
passage. No apparent changes occurred in the salt passage through-
out the operational period.
The mechanical operation of the tubular system was excellent.
No module failures were experienced over the entire 2,800 hr opera-
tion. This reflected the improvements made in tube construction
^
since the 1969 study.
In summary, a number of points can be made regarding tubular
system operation. The use of volume displacement rods is definitely
not recommended. The price paid in headless far exceeds the bene-
fits obtained. If higher velocities are required, it appears re-
circulation of brine would be the preferred alternative. With
regard to required velocities, it appears that a minimum velocity
of about 1.5 ft/sec (0.46 m/s) is desirable, since operation at this
velocity with the higher-flux—low-salt-passage modules was satis-
factory. It should be noted, however, that the recoveries during
Phase II were quite low (45-70 percent), and that operation at
higher recoveries may require higher velocities to offset the con-
centration polarization effects due to higher brine concentrations.
Additional study at higher recoveries is necessary to answer this
question.
115
-------
Table 43. SALT PASSAGE FDR TUBULAR STUDIES(15fl6) AT MOCANAQUA,
PENNSYLVANIA
Parameter
Calcium
Magnesium
Manganese
Total iron
Aluminum
Silica
TDS
Ferrous iron
Sulfate
Salt Passage -
Type 310 Membrane Type
Phase I
1.45
1.11
1.21
1.19
1.40
53.6
2.34
1.15
1.27
Percent
610 Membrane
Phase II
0.43
0.36
0.45
0.45
0.39
5.88
0.87
0.51
0.20
Analyses by Rex Chainbelt.
Note: Salt passage is related to salt rejection. Whereas rejec-
tion measures a membrane's impermeability to passage of ions, salt
passage is a measure of the relative permeability to passage of
ions. Therefore, salt rejection plus salt passage equals 100 per-
cent if both are measured in respect to the same initial concen-
tration.
116
-------
It is not known if the high initial flux loss experienced
during Phase I with the type 31D modules uas specific for the
modules utilized or a result of the higher salt passage. In any
event, low-salt-passage modules are definitely recommended for
both flux and product water quality considerations.
Comparing the flux history of Phase I 31D modules to the flux
history from the 1969 field testing, significantly lower flux
declines were noted in the present study. For example, greater
than SQ percent of the original flux was lost in t+QO hr in the
previous study compared to about ^+5 percent of the original flux
in the present study. This would indicate that the pretreatment
system did have some effect on the tubular system operation.
A more in-depth report of the hollow-fiber and tubular studies
at Mocanaqua is available , and a complete discussion of system
comparisons made from the results of this Mocanaqua study is pre-
sented in the "Discussion" section of this report.
Calcium Sulfate Fouling at Mocanaqua
Very little or no calcium sulfate fouling occurred at 75 percent
recovery since both the spiral-wound and hollow-fiber log-log flux
plots had shallow slopes and were linear. In contrast, the severe
fouling observed at 85 percent recovery was due to calcium sulfate
precipitation. Therefore, at some point between 75 and 85 percent
recovery, the solubility of calcium sulfate was exceeded and pre-
cipitation occurred.
At 75 percent recovery, the brine was concentrated four times
in relation to the raw feed; at 85 percent, the brine concentration
was 6.67 times that of the raw feed. Typical calcium and sulfate
values were used to generate Table Ub.
117
-------
Table 44. CALCIUM SULFATE MOLAR SOLUBILITY PRODUCTS
Recovery
75%
80%
85%
Concen-
tration
factor
i*.
5.
6.67
Raw
calcium
mq/1
120
120
120
Feed
sulfate
mq/1
800
BOO
800
Brine
calcium
mq/1
480
600
800
sulfate
mq/1
1920
3000
5340
Molar
solubility
product
2k x 10"5
47 x 10~5
111 x 10"5
As the recovery was increased from 75 to 85 percent, the product
of molar concentrations of calcium and sulfate in the brine in-
creased from 24 x 10~ to 111 x 10* . Since no CaSO, precipitation
occurred at 75 percent recovery, the limiting concentration was in
excess of 24 x 10~ ; if the point of precipitation were miduay be-
tween 75 and 85 percent recovery, this would correspond to a solu-
ior
-5
bility product near 50 x 10 . It is felt that precipitation
occurred in the solubility product ranqe of 35 and 50 x 10
NORTON FERRIC IRON STUDIES COMPARING HOLLOW-FIBER A1MD SPIRAL-WOUND
UNITS
Following termination of the RO study at Mocanaqua, EPA returned
two of the three hollow-fiber modules to Norton. These were permea-
tors 1 and 2 of the Mocanaqua 2-1 array which had operated for 1,832
hr at Mocanaqua at recoveries ranging from 58 to 66 percent. Also
returned to Norton was the 4 K spiral-wound unit which had accumu-
lated 2,454 hours of 75 percent recovery operation at Mocanaqua.
At Norton, the hollow-fiber studies were conducted in two phases.
Phase I consisted of the two first stage permeators from Mocanaqua
which were operated in parallel. During Phase II, three new perme-
ators were operated in a 2-1 array similar to the Mocanaqua Phase II
study.
Hollow-Fiber Studies - Phase I
In the parallel array, recoveries of the individual permeators
could be independently varied. This allowed direct comparison of
118
-------
fouling trends as related to brine concentration. Since minimum
brine flows were not a problem with hollow-fiber systems, recycling
brine to maintain a minimum floui was not felt necessary by the man-
ufacturer.
Differential pressure (the pressure loss across a module) is an
indicator of fouling in a permeator. Although the normal differ-
ential pressure (AP) fcr a hollow-fiber permeator is 1G psi
2
(69 kl\J/m ), the A p of the two permeators at the beginning of the
Norton study was UB psi (338 kl\l/m ). Apparently the fouling ob-
served at Mocanaqua had not been completely removed before the
Norton study began.
Operation of the modules on Grassy Run water began at approxi-
2
mately 75 percent recovery and ^+00 psi (2758 kl\J/m ). These condi-
tions were maintained for the first 5QO hr (2,325 total hours) of
operation. During this period,AP increased from 50 to 90 psi
2
(3^5 to 621 kf\l/m ) in each permeator, flux declined rapidly, and
two sodium hydrosulfide flushes were needed to maintain performance
(Figures 26 and 27). Typical operating parameters for the permeators
during this period are given in Table ^5. The log-log flux decline
slope for the first 315 hr of the 500 hr period was -.035. In the
remaining 185 hr, the slope significantly increased to -0.^5 in per-
meator number 2. During the next 750 hr of operation the AP and flux
decline continued to increase even though the recovery had been low-
ered to 50 percent. The rate of decline was significantly greater
in permeator 2 than in permeator 1.
A sodium hydrosulfide—BIZ combination flush dramatically re-
duced the AP- Fouling continued, however, despite the 50 percent
recovery rate. Salt rejections decreased with each sodium hydro-
sulfide flush.
In attempts to control the fouling, several variables were in-
vestigated to determine their relationship to the problem. Bacteri-
ological effects were studied by LJU disinfection of the raw feed
119
-------
Q
UJ
C£
ioo4-
50-)i
T>
c
D
0)
C
O
O
D
TJ
* 1.04-
o
O)
3.04-
2.0
• PERMEATOR 1
© PERMEATOR 2
-H 1-
0.0
220
440
660
1540
880 1100 1320
ELAPSED TIME, hours
Figure 26
Flux and AP history for the hollow-fiber phase I study at Norton
-------
o
o
C
O
rv)
O
TJ
CM
O
O>
1
10
-o
^
o
LOG-LOG SLOPE=-0.035
I
I
I
I
I
111 I
- aPERMEATOR 1
*. ©PERMEATOR 2
I I I
567
2 3 456789 100 2 3 456789 1000 23 4
ELAPSED TIME AT NORTON, hours
NOTE: 1 gal/ft2/day = 40.7 Iiter/m2/day
400 psi = 2759 kN/m2
77 °F = 25°C
Figure 27
Flux trends during the two permeator hollow-fiber phase I study at Norton
-------
Table 45. OPERATING PARAMETERS FDR NORTON TWO PERMEATOR HOLLOW-
FIBER STUDY AT 72 PERCENT RECOVERY
Parameter
Raw water feed flow, gpm
Product water flow, gpm
Brine water discharged, gpm
Brine water recycled, gpm
Water recovery, percent
Feed pressure, psig
Feed temperature, °F
2
Tube one flux, gal/ft /day @
2
Tube two flux, gal/ft /day @>
Length of run, hours
Date of run
Value
No. 1
2.435
1.763
.672
0
72. 4
407. S
60.2
400 psi & 77°F 2.601
400 psi & 77°F 2.576
Data thru 500
September 23 - October Ik
No. 2
2.415
1.750
.665
0
72.5
hours
, 1971
All values are means from 23 data sets.
Note: To convert flux (gal/ft2/day @ 400 psi and 77°F) to liters/
2 2
m /day @ 2758 kN/m and 25°C, multiply by 40.67; to convert gallons
per minute to liters/second, multiply by 0.063; and to convert psi
D
to kN/m2, divide by 0.145.
122
-------
uater, and calcium sulfate concentration and in-module turbulence
were studied by lowering the recovery and thus increasing the
brine floiu rate. Mane of these factors mere successful in flux
stabilization, however. Acid injection to lower the feed pH from
2.8 to 2.5 uas attempted at 1,500 hr (3,332 hr total on membrane)
elapsed time to study the possibility of iron precipitation. As
illustrated in Figures 26 and 27, acid injection uas relatively
successful in flux stabilization, thus confirming the probability
of iron fouling. However, acid was so high that the supply of acid
at Norton was exhausted in 2 weeks. It required 0.0001 gal of acid
per gallon of water treated to lower the influent pH from 2.8 to
2.5 (0.12 ml/1 treated).
Since spiral-wound units had performed successfully on the
Norton water in the past, it was difficult to understand the inabil-
ity of the hollow-fiber system to cope with the ferric water- To
ensure that some unknown condition in the water would not also
affect the spiral system, the relatively dilapidated 10 K spiral
unit,which had not operated since June 1970, was restarted using
the same modules as were used in 1970. The 10 K unit operated
alongside the hollow-fiber unit from September through December
1971 for a total period of 1,094 hr. During this period, the 10 K
2
operated at 400 psi (2758 kN/m ) and approximately 65 percent re-
covery and gained flux in each of the five tubes. At the same time,
the hollow-fiber unit was fouling severely.
At the end of the 10 K test, a sodium hydrosulfide flush of the
spiral system failed to significantly improve flux. The increase
in flux observed over the 1,094 hr period was attributed to gradual
removal of fouling that had occurred during the 1970 neutrolosis
tests (the last time it uas operating).
After approximately 2,200 hr of operation at Norton (4,000 total
hr) tests on the two hollow-fiber permeators were discontinued when
a satisfactory pressure differential and flux could not be maintained
even at low recoveries. The difference in flux stability of the per-
meators between the Mocanaqua site and Norton is readily apparent in
123
-------
Figure 28 which is a log-lag plot including both sites. The single
significant factor in the hollow-fiber test was that acid injection
to control influent pH at 2.5 was absolutely necessary to maintain
any operation of hollou-fiber permeators on the Norton water
(pH 2.8).
The manufacturer requested one of the permeators to determine
cause of fouling. In return, they supplied three new permeators
to be installed in a 2-1 array as uas used in Mocanaqua.
Hollow-Fiber Studies Phase I_I
Testing on the 2-1 array began January 31, 1972, and continued
uith relatively stable fluxes as long as hLSO, uas injected to main-
tain a feed pH of 2.5. After 231.1 hr of operation, the pH probe
line fouled and stopped flou through the probe. The influent pH
rose from 2.5 to 2.8 and AP across permeators 1 and 2 increased
from 13 psi to 11D psi in approximately 8 hr. Flux, when corrected
for pressure losses, dropped roughly 10 percent in the same 8 hr
period. Permeator 3 uas not affected by the influent pH as, even
without acid adjustment, the pH into permeator 3 uas belou pH 2.5
since it received brine from permeators 1 and 2.
A log-log plot of the flux of each of the three permeators is
given in Figure 29.
A sodium hydrosulfide flush of permeators 1 and 2 uas moderately
effective on permeator 1, but a failure occurred in permeator 2.
The feed distribution tube, made of polyethylene, collapsed during
the flush and allowed the "0" ring seals to fail. Rau water went
directly from the feed into the brine line bypassing the membrane
altogether. The manufacturer repaired the permeator on-site,
flushed it, and restarted the run but a high pressure loss again
recurred across permeators 1 and 2. The manufacturer took both
permeators back to further investigate the failure and fouling and
supplied two new ones to continue the test. Operating parameters
for the study are given in Table ^6. Typical chemical analyses are
121*
-------
4
30
0)
c
'« 20
Q.
0
o
c 10
° 9
U_
O
O -j
rv
K 6
•- @> e
(VI b
en >~
o 4
U
CS o
— J
*"*-
"""^
O
™ 2
X
U
u_
1
—
NORTON
-f ftrtOTANAOHA Tr*;T
"~ O
^^
_ ^J
NOTE:
01
>
o
U
a>
gx
~V
3-D — D a_0— c
n
>|
^
-C
,^
^5
-i n ni
U
^
•-
*o*
fr?
J
•J
r *4D
w
0)
•^
"-
3ftr — c
TJ
01
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i ea tor
t
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i°T
•*
•<»•
o
to
CM
O
Z
-C
V)
D
0
CM
1
1 gal/ft2/day = 40.7 Iiter/m2/day |
400 psi = 2759 kN/m2
77 °F = 25°C
1 1 1 1 1 I I I 1
S-l
O
o
_
Z
r-
V)
3
u-
^^S-D
CNO
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1 1
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i . i
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-DO:
ai
a "S
c ai ~
'^ L^
E
3 ^
1 ^
•A*
i i i i i
4
3
2
i
1
9
8
7
6
5
4
3
2
10
56789 100
200 300 400 600 800 1000
ELAPSED TIME, hours
2000 3000 4000 5 67891
Figure 28
Flux history for the two first-stage hollow-fiber permeators
-------
cn
CM
cs*
10.- . o« --D
9
8
7
6
_ 5
0)
c 4
VJ
a 3
0
O
-o 2
c
a
u.
o
K
^
^^^
- LOG-LOG SLOPES X ^ 2 1 NEW FIRST STAGE
DURING FIRST 200 MRS. - £ E = PERMEATORS
TUBE 1 = -0.047 O
TUBE 2 = -0.050 J5
TUBE 3 = -0.028 ~°
OVERALL TUBE 3 SLOPE = -0.052 5
_ u
X
*-^= *=fc*='-t»K
'
NEW FIRST
STAGE PERMEATORS ^
-
^
_
J
JC
t/i
n
0
a
a>
"^— «^
"•
«
0
o
© Log-Log Slope = -0. 083 •-
:&%-• — — Q c
t (LOWER GRAPH) -
_c
- 1
vt
N 0
03 12
Q)
0)
^
V
^
™-
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_
—
(Permeator Failure) "~
A
V ™
Log-Log Slope = -0.090
1 1 1 1 I 1 i 1 1 1
I 1
—
— --— » TUBE 1
-—--©TUBE 2
"TUBE 3
NOTE:
1 gal/ft2/day = 40.7 liter/m 2/day
400 psi = 2759 kN/m2
77°F = 25°C
1 1 1 I i 1 1 1 III!!!
9
8
7
6
5
4
3
2
1
9
8
7
6
5
4
3
1
10 2 3 4 5 6 7 8 9 100 200 300 4 56789 1000 2 3 4567891
ELAPSED TIME, hours
Figure 29
Flux trends for 6K hollow-fiber phase H study @ 69.7 percent recovery
-------
Table 46. OPERATING PARAMETERS FOR NORTON HOLLOW-FIBER 3-PERMEATOR
PHASE II STUDY AT 70 PERCENT RECOVERY
Parameter Value
Ram water feed flow, gpm 5.509
Total product flow, gpm 3.869
Product flou, permeator #1, gpm 1.303
Product flow, permeator #2, gpm 1.387
Product flow, permeator #3, gpm 1.179
Brine water flow through 1&2 (each), gpm 1.409
Brine water discharged (#3), gpm 1.64Q
Recovery - permeator #1, percent 48.0
Recovery - permeator #2, percent 49.6
Recovery - permeator #3, percent 41.8
Total unit recovery, percent 70.2
Feed pressure - unit, psig 400.0
Feed temperature - unit, °F 44.6
Permeator one flux, gal/ft2/day @ 400 psi net & 77°F 2.195
Permeator two flux, gal/ft2/day @ 400 psi net & 77°F 2.337
Permeator three flux, gal/ft2/day @ 400 psi net & 77°F 2.356
Length of run, hours 279.1
Date of run January 31-February 15, 1972
All values are means from 9 data sets.
Note: To convert flux (gal/ft2/day @ 400 psi and 77°F) to liters/
m2/day @ 2758 kN/m2 and 25°C, multiply by 40.67; to convert gallons
per minute to liters/second, multiply by 0.063; and to convert psi
to kN/m2, divide by 0.145.
127
-------
given in Table V7. The high hollou-fiber rejections are significant.
The manufacturer reported that manufacturing defects uere responsible
for the module failure following the sodium hydrosulfide flush.
The tuo new permeators uere installed at 279 hr elapsed time on
the unit. Careful modifications of the pH control system uere made
to insure that the pH probe uould not foul as before and operation
of the hollou-fiber system uas resumed.
Idithin 20 hr, a severe rain washed sediment from a neu mine road
into Grassy Run. An immediate flux loss occurred in the tuo first
stage^permeators. Correspondingly, the AP increased from 5 psi to
"* 2
62 psi (34.5 to 428 kl\l/m ). The third permeator uas unaffected.
The spiral-uound k K unit, operating alongside, suffered no flux
loss nor AP increase during the period.
A reverse flush uas partially successful in restoring flux and
2
reducing AP (from 62 doun to 35 psi) (428 to 241 k(\l/m ). After a
feu additional hours of operation, AP lowered to a normal value of
9 psi and flux again increased (though still not back to normal).
After a feu more hours of operation, houever, the trend reversed
and AP increased to near 70 psi and flux continued to drop. At
472.6 hr elapsed time (193.1 hr on permeators 1 and 2), testing uas
terminated as very little improvement in AP or flux had occurred in
permeators 1 and 2. Houever, permeator 3 uas still performing uell.
A one-hour reverse flou BIZ flush uas unsuccessful in reducing AP
or increasing flux in any of the permeators. The flux performance
of these permeators is included in Figure 29.
In all the hollou-fiber studies at (Morton, flux and AP stability
of the first stage permeators were unsatisfactory. Houever, the
second stage permeator performance uas significantly superior to the
first stage performance even though the second stage was receiving
uater with much higher pollutant concentrations.
Since the Phase I IMorton tests indicated acid injection uas
necessary to stabilize flux, it uas deduced that iron precipitation
128
-------
Table 47. CHEMISTRY ANALYSES FOR NORTON STUDY (1972)
pH Cond. Acidity Calcium Magnesium Iran Aluminum Manganese Sulfate
Hollou Fiber 6K Unit - Phase II
Acidified raw feed
Brine (from 1&2)
(Feed to #3)
Final Brine
Product #1
Product #2
Product #3
Rejections #1
Rejections #3
Spiral Wound
Raw Feed
Blended Feed
Brine
Total Product
Product #1
Product #2
Product #3
Total Rejections
2.6
2.3
2.1
3.8
3.8
3.7
2.7
2.5
2.4
3.6
3.9
3.9
4.0
1570
2950
5600
27
48
64
98.3%
97.8%
1800
3200
4400
55
60
55
48
98.3%
800
1520
2790
55
20
14
93.1%
99.1%
630
1370
2050
10
8
7
10
99.3%
96
200
330
<. 1
<.l
<.l
99.9%
99.9%
110
220
320
0.4
0.1
0.2
0.1
99.8%
29
56
100
<.l
<.l
<.l
99.7%
99.8%
30
68
96
0.1
0.1
0.1
0.1
99.9%
110
220
400
0.2
0.2
0.2
99.8%
99.9%
140
290
420
0.24
0.30
0.25
0.12
99.9%
36
70
120
<.l
<.!
<. 1
99.7%
99.9%
43
90
140
0.50
0.58
0.56
0.25
99.4%
4.0
7.7
13
0.2
0.2
0.2
95.0%
97.4%
3.3
8.1
14
<.01
•^.01
<.01
<.Q1
99.9%
1100
2300
2920
<1.0
7.0
7.7
99.9%
99.7%
810
1820
2800
3.5
3.5
2.7
2.7
99.8%
All units in mg/1 except for conductivity (micromhos/cm) and pH.
-------
was causing the observed fouling. This deduction was further rein-
forced in the first stage of Phase II tests when the pH probe fouled
and an immediate flux loss occurred. However, when the siltation
problem during the latter part of Phase II caused an immediate AP
increase, some additional insight to the nature of the fouling was
gained. Since 10 micron filtration preceded the RO unit, the fouling
particles were less than 10 microns in size and probably were col-
loidal in nature. Possibly, the fouling seen earlier during Phase I
was largely colloidal deposition reinforced by iron precipitation.
A first-stage permeator was opened and visually inspected at the
end of the Phase II tests. The outside of the fiber bundle, where
brine concentrations were the greatest, showed absolutely no fouling
as the fibers were extremely clean. Upon dissecting the bundle, the
fibers grew darker toward the central distributor tube through which
the ratj water enters. The fibers immediately surrounding the central
distributor were coated with a brown film resembling mud. Samples
taken throughout the bundle were sent to West Virginia University
for X-ray analyses. Significant quantities of allophane-like (poorly
crystalline) material composed of alumina and silica were present on
17
the membrane. The alumina/silica ratios suggested the existence
of significant quantities of clays. This result confirmed the diag-
nosis of colloidal fouling. Also present on the membranes were
large amounts of metallic iron particles which were attributed to
the carbon steel connecting rod of the Moyno high-pressure pump.
The connecting rod sheared at the end of the hollow-fiber test.
Dr. Smith of West Virginia University also investigated the use of
a combination ultrasonic and Calgon cleaning technique for removal
of the residue on the membrane. Calgon served as an effective
wetting agent and the ultrasonic treatment completely removed the
coating from the membrane surface. However, it is not known whether
this technique would be applicable in a module which had not been
dissected.
The difference in hollow-fiber flux stability at Mocanaqua and
the instability at Norton is attributed to the fact that Grassy Run
130
-------
at (Morton is a surface stream subject to siltation and sewage loads
not seen in the underground mine discharge at Mocanaqua. Even though
ferric iron was observed to be more difficult to treat than ferrous,
it is felt that acid injection to approximately pH 2.5 ujill control
iron precipitation.
The inability of the hollou-fiber system to tolerate colloidal
or particulate matter less than 10 microns in size must be deemed a
major disadvantage and would significantly limit the application of
hallow-fiber systems on acid mine streams unless the problem can be
overcome.
Spiral-Wound Studies
Although the U H spiral system was returned to Norton in Novem-
ber 1971, logistical problems delayed resumption of testing until
January 3D, 1972. This 2 mo down time allowed considerable relaxa-
tion to occur in the membrane which had operated for 245^ hr at
Mocanaqua. Consequently, when testing began at Norton, the flux
2 2
rates were in the range of 12 gal/ft /day (^90 1/m ) (higher than
at the end of the Mocanaqua study). In addition to membrane relaxa-
tion, corrections for temperature and osmotic pressure at the new
site may have resulted in slightly higher flux values.
The osmotic pressure-conductivity relationship for the Norton
water is shown in Figure 30.
Operation of the b K spiral system at Norton was at UOO psig
(2758 kl\l/m2), 70 percent recovery, and better than 10:1 b/p flow
ratio. The unit accumulated an additional 19<+6 hr of operating
time to bring the total membrane time to ^00 hr.
Flux performance is shown two ways in Figure 31: in the top plot,
the complete flux history for tubes 1 and 3 is shown; in the lower
plot, operating time at Norton is presented independently. A least
squares regression analysis provided a log-log line of best fit for
the Norton operation with a slope of -0.036 for tube 1 and -0.016 for
tube 3. Tube one's slope, though very reasonable, was significantly
131
-------
VjJ
ro
._ 30
20
in
to
LU
tt
a.
u
CO
O
10
OP = 0.308 C
.498
ACID INJECTION, OP = 0.185 C
.498
I
I
1
I
cs
200
150
100
50
Of.
ID
co
CO
LU
Of.
Q_
to
O
1000 2000 3000 4000 5000
CONDUCTIVITY (C)MICROMHOS/cm
Figu re 3 0
Osmotic pressure - conductivity relationship of Grassy Run at Norton
-------
1 2 34567891 2 34567891 2 34567891
9
8
» 6
c 5
"> 4
Q. 4
O
0 3
"^
TJ
C 2
O
u-
o
10
©/ 9
8
0 7
~Q 6
cs 5
^^ j
O
D) 3
X
3 2
^J
u_
1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 L
NORTON
(/)
LU
< 00 >-
- O X tl
° Z -
< S <
MOCANAQUA STUDY ^O?
o ~r
5 "~
S^O
Q
IU
SLOPE = -0.012
A A ft — A — 2S — A — & A & A £. Jl£.A iJ. JL^T^J^D,
SLOPE = -0.009 ° ° ^ W °°° °° °° °®^^1
STUDY
(SEE
BELOW)
5
o —
_l
u_
N —
CO
Of _
O
X
^^Sp
•^
- — i
-
-
NORTON OPERATION ONLY
NOTE:
1 GAL/FT2/DAY = 40.7 LITER/m2/DAY
400 psi = 2759 kN/m2
77°F=25°C
_
SLOPE = -0.036
S A y«^ A ^ £ A A A A ft r iSiAyvA A -
vj o W" w — w — w — '*' o * ' * * * fvA rVi LJ ."jifaat
0 SLOPE = -0.016 ^" U^ '-UjtS&g
1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1 1
«•
^
OTUBE1
S ATUBE3 ~
i
Isl
CO ~"
cc
O
I
1 —
L 1 1 1 1 1 1 1
9
8
7
/
6
5
4
3
1
9
8
7
6
5
4
3
2
10
56789 100 2 3 456789 1000
ELAPSED TIME, hours
Figure 31
Total 4K spiral unit operating history
5 67891
-------
greater than the -O.D10 slope observed on the same modules at
Mocanaqua. It is felt that the increase in slope uas directly re-
lated to the fact that Grassy Run is a surface stream subject to
colloidal loads far higher than the deep mine discharge at Mocanaqua.
This contrast i.,
-------
Table 48. OPERATING PARAMETERS FOR NORTON SPIRAL-tdOUND 4K STUDY
AT 69.6 PERCENT RECOVERY
Parameter Value
Raw water feed flow, gpm 5.076
Product water flow, gpm 3.531
Brine water discharged, gpm 1.545
Brine water recycled, gpm 6.577
Minimum brine/product flow ratio, ratio/module 10.6:1
Maximum brine/product flow ratio, ratio/module 21.6:1
Water recovery, percent 69.6
Recovery of blended feed, percent 30.3
Feed pressure, psig 400.1
Feed temperature, °F 59.2
Tube one flux, gal/ft2/day @ 77°F & 400 psi net 13.68
Tube two flux, gal/ft2/day @ 77°F & 400 psi net 13.32
Tube three flux, gal/ft2/day @ 77°F & 400 psi net 13.04
Length of run, hours 1946
(4400 total hours on membrane)
Date of run January 30, 1972 - May 17, 1972
All values are means from 53 data sets.
Note: To convert flux (gal/ft2/day @ 400 psi and 77°F) to liters/
m2/day S 2758 kN/m2 and 25°C, multiply by 40.67; to convert gallons
per minute to liters/second, multiply by 0.063; and to convert psi
to kN/m2, divide by 0.145.
135
-------
spiral system under both ferrous (Mocanaqua) and ferric (Norton)
conditions. The spiral system uas significantly more tolerant to
colloidal loads than the hollow-fiber system as shouin by the satis-
factory spiral system operation on the Norton water- However, the
increase in the spiral system's rate of flux decline at Norton as
compared to Mocanaqua uias directly attributed to colloidal fouling.
Importantly, the rate of spiral flux decline uias still very accept-
able and could be controlled quite easily through periodic flushing.
No decrease in salt rejection capability was noted on the spiral
unit during the entire ^00 hr of operation.
Operation of the spiral system at high b/p flow ratios (10:1)
Q
and lower pressure (^00 psi - 2758 kN/m ') produced significant im-
provements in flux stability compared to the 1970-71 3D13 hr Norton
k h study where approximately 25 percent of the flux was lost in the
first 500 hr.
POST TREATMENT OF PRODUCT WATER
In an effort to produce a product of potable quality, product
samples from the early part of the spiral testing and from the hollow-
fiber Phase II study were neutralized to pH 7.5 and analyzed. The
three critical parameters were pH, iron, and manganese. As shown in
Table i*9, neutralization effectively increased pH and removed iron
but manganese levels remained unchanged and in excess of the D.05
mg/1 limit. Neutralization to pH 9-10 would have been required for
19
manganese removal. In that case, reacidificatian would have been
necessary to reduce pH to acceptable limits of pH 6.0 to 8.5. A
quick neutralization to pH 10 confirmed removal of manganese to
potable standards. A more complete discussion of this problem is
presented in the Discussion, Section VI, of this report under the
subsection Significances of Rejection.
136
-------
Table ^9. EFFECT OF NEUTRALIZATION ON RO PRODUCT QUALITY
Spiral-Wound
pH
Conductivity
Acidity
Alkalinity
Calcium
Magnesium
Iron
Aluminum
Sulfate
Manganese
Data 2/8/72 -
pH
Manganese
Data 3/20/72
Product
3.8
100
58
0
0.5
0.2
0.38
0.10
7.0
0.3
Norton Study
Product
i+.O
0.06
- Norton Study
Neutralized Product
7.5
60
0
10
5.6
0.2
0.07
0.08
7.7
0.3
Spiral -Wound
Neutralized Product
10.0
0.001
Hoi low-Fiber
Product Neutralized Product
3.9
65
56
0
0.2
0.1
0.07
<0.1
5.7
0.2
7.5
55
0
5
3.2
0.1
0.005
< 0.1
8.3
0.2
All units in mg/1 except for conductivity (micromhos/cm) and pH.
-------
SECTION V/I
DISCUSSION
CALCIUM SULFATE PRECIPITATION - MAXIMUM RECOVERY PREDICTION
In each of the spiral-wound studies made at the various AMD
sites, one result was significant—the limiting factor in high re-
covery reverse osmosis operation was calcium sulfate precipitation.
Gulf Environmental Systems presented a discussion of the CaSO^
problem and suggested the following method to predict precipitation:
/Pmc = 3.0 to 4.0 uhen fouling occurs, where
V Ksp
Pmc = Product of molar concentration of calcium
and sulfate in the brine.
Pmc = (Mg/1 calcium '- 40.08) x (Mg/1 SO^ 7 96.06) x 10~6
Ksp = Solubility Product of Calcium Sulfate in distilled
water where solubility & 2000 mg/1 and Ksp = 2.16
x 10~4
Unfortunately, a broad range of 3.0 to 4.0 was not adequate in
predicting RO recovery with any degree of accuracy.
Using Gulf's approach, data from each site mentioned in this re-
port were evaluated and a judgmental estimate was made of the maximum
sustainable recovery level at each site. This engineering estimate
was based solely upon experience and was thus empirical in nature and
subject to error and disagreement.
Since the brine samples from each test were supersaturated in
calcium sulfate, precipitation occurred prior to analysis. It was
felt that using raw feed values and calculating brine concentrations
based on recovery would give more reliable values for calcium and
sulfate concentrations. For example, if the RO unit were operated
at 75 percent recovery, the brine values would be concentrated four
times in relation to raw feed values. Calculations of the brine
concentration were then made based on the assumed maximum recovery.
138
-------
The major argument against Gulf's method is that Ksp is a value
for calcium sulfate solubility in distilled water. A Ksp for highly
polluted brine uith all involved ionic competitions would be a
significantly different value than that for distilled water.
Earlier work at Gulf included formulations by Marshall, Slusher.
18
and Jones for correcting Ksp of CaSO^ for ionic strength. Although
the work was at higher temperatures and sodium chloride solutions,
Gulf felt the relationships were generally valid for RO applications.
The ionic strength (I) of a solution is defined as:
, -, 2
Mi = molar concentrations of individual ions
Zi = ionic charges
Marshall, Slusher, and Jones related ionic strength (I) to Ksp
for calcium sulfate as follows:
Ksp = 1.8 x 10"3 (I) n*75
Therefore, n second approach mas used where -JPrnc/Hsp UBS calcu-
lated using Ksp corrected for ionic strength.
Table 50 presents a summary of all tests along with estimates of
maximum sustainable recoveries at those sites and corresponding
values of v/Pmc/(2.16 x 1D~ ) and >/Pmo/Ksp (corrected).
Table 51 presents a summary of chemistry analyses at all sites.
The yPmc/Ksp corrected for ionic strength was calculated from
these values.
It was felt that the results of Table 50 provided rough limits
for the calcium sulfate threshold of /Pmc/(2.16 x 10 ) = 2.0 and
7 Pmc/Ksp =1.2 (where Ksp was corrected far ionic strength).
Computer programs were then written to calculate the maximum
predicted recovery based on analyses of the raw feed water. The
program incremented recovery, calculated brine concentrations, and
solved 7Pmc/Ksp until limits of 2.0 (Ksp = 2.16 x 1D~*) or 1.2
(Kap corrected for ionic strength) were reached.
139
-------
Table 50. REVERSE OSMOSIS RECOVERY LIMITATIONS DUE TO CALCIUM SULFATE FOULING
Actual Values
Actual
Site recovery
Norton 10K - Test #1
Norton 10K - Test #2
Norton Neutrolosis-Test 4
Norton Neutrolosis-Test 5
Morgantown
Ebensburg #1
Ebensburg #4
Norton 4K - 3000 hr
Norton 4K - Neutralized brine
4K Mocanaqua #1
4K Mocanaqua #1
4K Mocanaqua #2
4K Norton (1972)
91.2%
84.8%
55.6%(b)
54.6%
50.0%
83.6%
53.2%
72.8%
50.0%
74.8%
83.9%
74.5%
75.0%
Raw
Ca
110
110
460(b
530
190
160
120
400
130
130
140
96
feed
810
850
} 4700 (b
J 3000 (b
10900
1640
1300
1100
3100
750
800
930
1060
/ Pmc
3.72
2.21
5 3.67
5 2.84
5.27
3.73
1.07
1.47
2.44
1.36
2.20
1.55
1.40
Calculated Values
/ Pmc Estimated
V Ksp maximum /• .
(corrected) recovery <
1.74
1.29
1.66
1.59
1.87
1.89
0.85
0.94
1.55
0.99
1.33
1.05
0.93
85%
85%
30%(b)
40%(b)
<1%
75%
75%
80%
20%
80%
80%
80%
85%
Mean
./Pmc '
J 2.16
2.18
2.24
2.33
2.15
2.66
2.45
2.00
1.99
1.53
1.71
1.77
1.98
2.33
2.10
/Pmc
\/Ksp
(corrected)
1.25
1.30
1.25
1.33
1.22(C)
1.45
1.26
1.14
1.16
1.14
1.16
1.22
1.28
1.24
Maximum sustainable recovery (estimated).
Blended feed values.
Excessive at any recovery.
-------
Table 51. SUMMARY OF RAW FEED CHEMISTRY ANALYSES
Site
Norton lOK-Test 1
Norton lOK-Test 2
Norton Neutrolosis
Test #4(a)
Norton Neutrolosis
Test #5(a)
Morgantown
Ebensburg #1
Ebensburg #4
4K Norton - 3000 "hr
4K Norton
4K Mocanaqua #1
4K Mocanaqua #1
4K Mocanaqua #2
4K Norton (1972)
Actual
recovery
91.2%
84.8%
55.6%
54.6%
50.0%
83.6%
53.2%
72.8%
50.0%
74.8%
83.9%
74.5%
75.0%
Cond.
1100
1200
5200
3000
7000
1500
1180
970
3200
1080
1100
1110
960
Acidity
630
540
2700
1150
5200
380
390
440
66
240
230
220
620
Ca
110
110
470
460
530
190
160
120
400
130
130
140
96
Mq
33
37
270
120
420
54
51
39
170
88
90
110
29
Total
iron
110
80
520
210
2300
135
130
130
1.3
77
80
100
115
Ferrous
iron
3
3
10
10
1300
100
96
3
0.1
64
70
73
3
Al
35
31
190
91
320
32
30
63
4.5
12
13
14
36
Sulfate
810
850
4700
3000
10900
1640
1300
1100
3100
750
800
930
1060
Blended feed values.
All units are mg/1 except for pH and conductivity (micromhos/cm).
-------
In Table 52, results of computer predictions can be compared with
the estimated maximum recovery for each site. Maximum recovery
predictions by both methods agree very well with each other and
uith the original estimate of maximum recovery.
Since agreement between both methods ujas close, use of
7PmcX2.16 x 10~4) = 2.0 is recommended since only calcium and sul-
fate determinations are needed to compute maximum recovery. Using
2.D as the limit, the following formula was derived to enable pre-
diction of maximum recovery:
R - 100 - D.D55 (Ca) x
where R = maximum recovery (percentage)
Ca - AMD feed calcium concentration (mg/1)
SO, = AMD feed sulfate concentration (mg/1)
This method of predicting maximum recovery is felt to be accu-
rate to H^ 5 percent recovery on acid mine drainage.
COMPARISON OF SPIRAL-LIOUND, HOLLOw-FIBER, AMD TUBULAR SYSTEMS
In order to compare RO systems, it was vital that all comparisons
be made on the same basis, i.e., under the same operating conditions.
For this reason, water flux, when corrected for osmotic pressure
(which corrects for water quality and recovery) and temperature,
served as an effective unit for comparing of membrane performance.
Water flux, however, did not compensate for efficient packaging of
the membranes in the RO system, and therefore was a poor basis for
comoaring Fa/stem performance.
For this report, system performance was evaluated on the basis
of product output per cubic foot of vessel volume per unit of time.
To arrive at this factor, water flux was divided by pressure vessel
volume.
Table 53 presents a summary of observed flux and productivity
data from the Mocangqua studies where spiral-wound, hollow-fiber,
and tubular systems operated on a side-by-side basis. Tubular and
Phase I spiral-wound data—although actual operation was at
-------
Table 52. COMPARISON OF PREDICTED MAXIMUM RECOVERY UJITH EMPIRICAL ESTIMATES OF MAXIMUM RECOVERY
Norton 10K - Teat 1
Norton 10K - Teat 2
Norton Neutrolosis - Teat
-------
Table 53. COMPARISON OF WATER PRODUCTION CAPABILITIES OBSERVED DURING MOCANAQUA STUDIES
Pressure Membrane
vessel Enclosed packing
volume membrane density
f ±3 araa Ft? Ft2/ft3
Avg. flux
Total
vessel
flux/da
Output per cubic foot of
vessel volume
per
per
Spiral-wound
(Phase I) 1.13
150
(19.28 @ 600) (2892 @ 600) (2559 @ 600) (1.78 @ 600)
133 12.86 1929 1707 1.19
Spiral-wound
(Phase II) 1.13
186
165
12.31
2290
2026
-F-
.c-
Hollow-fiber
(Phase
Tubular
(Phase
II)
II)
0.
0.
65
63
1500
16.9
2308
26.8
2.
(15.60
10.
48
@ 600)
40
3720
(264 @ 600)
176
5723
(418 @ 600)
280
3.
(0.29
0.
97
@ 600)
19
(a)At 77°F (50°C) and UOO psi net pressure.
33 22
Note: To convert ft to m , multiply by 0.028; to convert ft to m , multiply by 0.093; to
convert flux values (gal/ft2/day @ 77°F and kOQ psi) to l/mZ/day @ 25°C and 2758 kN/m2,
multiply by UQ.67.
-------
kl\l/m (600 psi)—ucre also normalized to 2758 kIM/m (UQQ psi)
to enable direct comparrson uith the holloui-fiber unit.
In terms of average flux, spiral-uound membranes uere clearly
superior uith 2758 kN/m2 (^00 psi) fluxes of 12.3 gal/ft2/day for
spiral versus 10. MD fnr tubular and only 2.<+S for hollou-f iber
(500 l/m2/day vs. ^23 vs. 100.8).
Because hollou-fiber permeators packed from 8-10 times as much
membrane in the same volume as the spiral system and 88 times as
much as the tubular system (see Packing Density, Table 53), the lou
specific flux of the hollou-fiber uas made up for by greater membrane
area. Although the hollou-fiber flux rate ranged from only 12 per-
cent to 20 percent tint of the spiral system, depending on the
spiral's operating pressure, the hollou-fiber product output per
cubic foot of vessel volume uas from 2.2 to 3.3 times spiral output
and from 1*4 to 21 times tubular output, again depending upon operat-
ing pressures.
The tubular system ranked louest in both flux and output per
cubic foot of vessel volume.
In Table 5^ are the relative costs for each system. Since a de-
tailed cost analysis uas beyond the scope of this report, initial
costs for purchase of one pressure vessel complete uith membrane uere
used. Dividing the initial cost by the observed output (gallons per
day of product) yielded the initial cost-per-unit-output figures
shoun in the table. Although prices and relationships observed
were valid for the Mocanaqua study, extrapolation of these figures
for large units uauld result in large errors. Other factors such
as harduare requirements uould vary uith each application and manu-
facturer and uere not included in pressure-vessel--membrane-package—
cost figures.
A third basis for comparison uas product quality. Rejections
uere calculated bv comparing the product concentration uith concen-
-------
Table 54. RELATIVE COST COMPARISONS FROM MOCANAQUA STUDY
en
System
Spiral-wound
Phase I
Spiral -mound
Phase II
Hollow-fiber
Phase II
Tubular Phase II
Cost for one
pressure vessel
and membrane
$ 850.(20)
I 850.(20)
$1000. (21)
$ 265.(22)
Observed output (gal. per
vessel per day @ 77° F
& indicated net pressure)
2892 @ 600
2290 @ 400
3720 @ 400
264 @ 600
Initial cost
per unit out-
put (gal/day)
$0.29
$0.37
$0.27
$1.00
Note: To convert gal/day to I/day, multiply by 3.785 and to convert $/gal/day to $/l/day,
divide by 3.785.
-------
trations entering the RD unit. A summation of system rejections is
presented in Table 55. Spiral-wound membranes held a slight edge
in rejecting ability.
The previously mentioned leaks during spiral-mound Phase II
studies were apparent in unit rejections (Table 55), but tube 3
rejections were of the same level as those from Phase I spiral
studies.
Under Mocanaqua conditions, the rejection advantage of spiral
membranes would be of little significance as product mater from all
three units would require additional treatment for pH, manganese,
and iron before drinking water standards could be met.
The final basis for comparison was the decrease of productivity
with time as evaluated by log-log flux decline slopes. In Table 56
are examples of log-log slopes (derived from Figures 23 and 25 and
Table 53) chosen to simulate comparable recovery conditions. In all
these examples, recoveries in the respective tubes or units were
near or below 60 percent.
Phase II spiral-wound system again had a slight advantage in
flux decline slope over the hollow-fiber systems; however, the
hollow-fiber slope was superior to Phase I spiral performance. The
tubular system's slope, calculated from the line of best fit of the
tubular log-log flux plot, was considerably steeper than either the
spiral or hollow-fiber slope.
Extrapolation of the flux curve to predict flux values at 3 and
5 years was necessarily based on the assumption that the log-log
flux decline slope remained constant. Validity of that assumption
is certainly open to debate and only sustained operation over that
period of time would prove or disprove it. If the assumption were
valid, the flux levels at 3 and 5 years of elapsed time are given
in Table 56.
-------
Table 55. COMPARISON OF MEMBRANE PERFORMANCE AT MOCANAQUA
00
System
Spiral-wound
Phase I
Spiral-wound
Phase II
Spiral-wound
Tube 3, Phase
Holloui-fiber
Phase I
Hollow-fiber
Phase II
Tubular
Phase I
Tubular
Phase II
Flux, gal/fW
day @ 77° F &
indicated pressure
19.28
@ 600 psi
12.31
@ 400 psi
11.58
II @ 400 psi
2.32
@ 400 psi
@ 400 psi
15.6
@ 600 psi
Rejections^)
Conduc- Acid-
tivity Ity
99.2 91.7
97.6 94.6
98.7
-
96.9 84.8
95.6 81.6
96.2
Cal-
cium
99.8
99.6
99.8
99.5
99.2
98.2
99.5
Magne-
sium
99.8
98.5
99.7
99.3
98.8
98.5
99.5
Total
iron
99.8
99.0
99.7
99.2
98.9
98.8
99.4
j Percent
Ferrous
iron
99.8
98.9
-
99.1
98.9
98.4
99.0
Alum-
inum
99.2
97.6
97.7
97.8
94.7
91.7
98.2
Sul- Manga-
fate nese
98.8
99.1 99.8
99.7 99.5
99.7 99.4
99.5
99.3
96.9 99.4
Sili-
con
95.1
-
90.0
Rejection = (Influent concentration-product concentration) x 100 •• Influent concentration.
22 2
Note: To convert flux gal/ft /day to 1/m /day, multiply by 40.67; to convert psi to kN/m , divide by 0.145.
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(a)
Table 56. PROJECTED MEMBRANE PERFORMANCEIB' - MOCANAQUA STUDIES
Flux ®fh} Log-log Predicted
100 nrs. °' flux de- flux after
Unit qal/ft^/day cline slope 3 years
Spiral-wound Phase I
Tube 1 21.5 -0.03^ 17.8
Spiral-wound Phase II
Tube 1 13.0 -0.012 12.2
Hollou-fiber Phase II
Tube 1 2.9 -0.015 2.7
Tubular Phase II 17.2 -0.063 12.1
Predicted
flux after
5 years
17.5
12.1
2.6
11.7
Ca)
Assumptions:
1. Log-log flux decline slope remains constant.
2. Salt rejection is assumed to remain constant.
Taken from log-log graph of flux versus time.
2 2
Note: To convert gal/ft /day to 1/m /day, multiply by ^0.67.
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SIGNIFICANCE OF REJECTIONS
Most important of the several factors that determine reverse
osmosis product quality are rau uiater quality, recovery level, and
membrane rejection caoability.
If uater of potable quality is required without posttreatment
of the product, then significant restrictions are placed upon the
mode of operation and characteristics of the RD unit.
Iron and manganese concentrations in potable water are restricted
by the U. S. Public Health Service to 0.3 and 0.05 mg/1, respectively.
Of all commonly appearing AMD constituents, iron and manganese are
the most critical for treatment to potable standards.
Since the membrane rejection ratio is constant, product quality
is directly dependent on concentrations on the brine (concentrated)
side of the membrane. Increasing recovery serves to increase brine-
side concentrations and in turn degrades product quality. Therefore,
for every rau feed concentration, it id possible to calculate the
maximum recovery that can be obtained without the product concen-
tration exceeding the U. 3. Public Health Service limit. A family
of operating curves has been developed for iron and manganese and
may be used to approximate this maximum recovery (Figures 32 and 33).
For example, if an influent water contained 50 mg/1 of iron and 5
mg/1 of manganese, the maximum recovery to meet potable standards
would be 30 percent for the iron criteria when using 99.5 percent
rejecting membranes. The same conditions allow a 66 percent recovery
before manganese limits are exceeded.
It is not necessary for the RO unit to reduce the iron and man-
ganese to this low level since the product water must receive post-
treatment in the form of neutralization to increase the pH to an
acceptable level. RO-treated water normally has a pH less than 5,
Neutralizing to pH 7 and filtering will remove residual iron, and
thus, the iron concentrations can be kept in acceptable limits. If
the iron is in the ferrous state, it will rapidly oxidize at pH 7,
150
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99.9% REJECTION
95.0%
(REJECTION RATE)
I I
10
2 4 6 8 10 20 40 60 80100 200
IN FLUENT CONCENTRATION, mg/l
Figure 32
Maximum operating conditions to obtain potable product
for iron limits of 0.30 mg/l
8
-------
U1
(V)
100
90
80
70
c 60
S 50
S. 40
£ 30
0% (REJECTION
RATE)
EJECTION
J
I
.2
.4
.6 .8 1.0 2 468 10
INFLUENT CONCENTRATION, mg/l
Figure 33
Maximum operating conditions to obtain potable product
for manganese limits of 0.05 mg/l
20 30 40 60 80
-------
and then it can be removed by filtering. To remove residual man-
19
ganese by neutralization, Hill states that neutralization to pH
9-10 is required. This neutralization in itself would exceed
normally acceptable pH limits and acidification of the uiater would
be needed following manganese removal.
In conclusion, assuming potable quality product water is re-
quired from the RD unit, membrane rejection is generally not sig-
nificant for iron removal since post neutralization is required
anyway. However, far AMD waters containing significant amounts of
manganese, the rejection capability is of vast importance in
achieving potable quality at minimum cost. Membranes with rejec-
tions below 95 percent would not appear desirable for AMD potable
applications.
If the RD system can be operated in a mode where the iron and
manganese can be reduced to an acceptable level by the addition of
a posttreatment step, then the unit can be operated at a high
recovery.
153
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SECTION VII
REFERENCES
1. Rusnak, A. and I. IMusbaum, Reverse Osmosis Field Testing on
Acid Mine Waters at Norton, tile at Uirqinia, Office of Saline
Water Contract No. 14-01-0001-1243, Gulf Environmental Systems
Report No. GA-8796, San Diego, California, August 196S.
2. Riedinger, A. B., Reverse Osmosis Field Testing on Acid Mine
Waters at Norton, West Virginia, Office of Saline Water Con-
tract No. 14-01-0001-1836, Gulf Environmental Systems Report
No. GA-91S1, San Diego, California, January 1969.
3. Gulf Environmental Systems Company, Acid Mine Waste Treatment
Using Reverse Osmosis, Environmental Protection Agency, Report
No. 14010 DYG 08/71, Washington, D. C., August 1971.
4. Rex Chainbelt, Inc., Treatment of Acid Mine Drainage by Reverse
Osmosis, Environmental Protection Agency Report No. 14010 DYK
03/70, Washington, D. C., March 1970.
5. Riedinger, A., and J. Shultz, Acid Mine Water Test at Kittanning,
Pennsylvania, Research and Development Progress Report No. 217,
Office of Saline Water, Washington, D. C., 1966.
6. E. I. DuPont de Nemours & Company, Technical Bulletin No. 100,
Wilmington, Delaware.
7. Salotto, B. V., et al., Procedure for Determination of Mine
Waste Acidity, paper given at the 154to National Meeting of the
American Chemical Society, Chicago, Illinois, 1966.
8. Environmental Protection Agency, Methods for Chemical Analysis
of Water and Wastes, 1971.
9. U. S. Steel Corporation, Sampling and Analyses of Coal and Coke
and By-products. Third Edition, 1929. -—-————-
10. Gulf General Atomic, Inc., Reverse Osmosis Principles and Appli-
cations, San Diegof California, October 1969.
11. Hill, Ronald D., R. C. Wilmoth, and R. B. Scott, Neutrolosis
Treatment of Acid Mine Drainage, paper presented at 26*6 Annual
Purdue Industrial Waste Conference, Lafayette, Indiana, May 1971.
154
-------
12. Wilmoth, R., and R. Hill, Neutralization of High Ferric Iron
Acid Mine Drainage, Federal Water Quality Administration,
Report No. li+01D ETV 08/70, Washington, D. C., August 1970.
13. Mason, Donald G., Personal communication, August 1971.
1*4. Sleigh, James H., Personal communication, August 1971.
15. Wilmoth, R. C., D. G. Mason and M. Gupta, Treatment of Ferrous
Iron Acid Mine Drainage by Reverse Osmosis, paper presented at
Fourth Symposium on Coal Mine Drainage Research, Pittsburgh,
Pa., April 1972.
16. Rex Chainbelt, Reverse Osmosis Demineralization of Acid Mine
Drainage, Environmental Protection Agency, Report No. 1^010
FQR 03/72, Washington, D. C., April 1972.
17. Grube, Walter E., and Dr. R. M. Smith, West Virginia University,
Personal Correspondence, May 17, 1972.
18. Marshall, W. L., R. Slusher, and E. V. Jones, "Aqueous Systems
at High Temperature, XIV. Solubility and Thermodynamic Rela-
tionships for CaSO^ in Nacl-H2Q solutions from <+.0° to 200°,
C, 0 to *+ Molal Nad." Journal of Chemical Engineering.
Data 9,187 (1965).
19. Hill, Ronald D., Mine Drainage Treatment, State of the Art and
Research Needs, U. S. Dept. of the Interior, Federal Water
Pollution Control Administration, Cincinnati, Ohio, December
1968.
20. Sleigh, James H., Gulf Environmental Systems Company, Personal
Communication, December 1971.
21. Potter, H. G. Jr., E. I. DuPont de Nemours, Inc., Personal
Communication, July 1971.
22. Mason, Donald G., Rex Chainbelt, Inc., Personal Communication,
December 1971.
155
-------
SECTION Will
LIST OF INVENTIONS AND PUBLICATIONS
INVENTION
A patent application (No. 213117) has been filed for the neu-
trolosis process. The title is "Reverse Osmosis - Neutralization
Process for Treating Contaminated Waters" by Ronald D. Hill,
Roger C. Uilmoth, and Robert B. Scott. As of this report, the
patent is pending.
PUBLICATIONS
The following list of presentations and publications resulted
from portions of the uork included in this report:
"Neutrolosis Treatment of Acid Mine Drainage" by Ronald D. Hill,
Roger C. Uilmoth, and Robert B. Scott, a paper presented at the
Purdue Industrial Waste Conference, Lafayette, Indiana, in May 1971;
"Treatment of Ferrous Iron Acid Mine Drainage by Reverse Osmosis"
by Roger C. Idilmoth, Donald G. Mason, and Mahendra Gupta, a paper
presented at the Fourth Symposium in April 1972;
"Mine Drainage Pollution Control by Reverse Osmosis" by Roger
C. Ulilmoth and Ronald D. Hill, a paper presented at the AIME Fall
Meeting, Birmingham, Alabama, in October 1972;
and "Mine Drainage Pollution Control Via Reverse Osmosis",
Mining Engineering. March 1973, page kS-kl, by Roger C. Wilmoth
and Ronald D. Hill.
156
-------
SECTION IX
GLOSSARY
Flux - A measure of productivity or permeability; the rate of prod-
uct flow through the membrane, usually expressed as gallons per day
per square foot of membrane area under specified conditions of tem-
perature and pressure.
Log-Log Flux Decline Slope - Even in pure water (nonfouling) systems,
reverse osmosis membranes lose flux with time. This flux loss is
linear when plotted on log-log paper. Log-log flux slopes of test
runs are indicative of the fouling that may be occurring, its sever-
ity, and its rate as compared with normal pure water values.
Pressure Drop (AP) - The pressure loss across a module or tube in
an RO unit due to hydraulic restriction in the brine channel and
piping. Increases in A P are rough indicators of fouling.
Recovery - The percentage of the raw water fed to the reverse osmo-
sis unit that results as product.
Reverse Osmosis - Flow through a semipermeable membrane where the
direction of flow is from the concentrated solution to the dilute
solution. Such a flow is induced by pressure applied to the con-
centrated solution.
Salt Rejection - A measure of a membrane's ability to selectively
allow pure water to pass through but reject the passage of impur-
ities; a measure of a membrane's impermeability with respect to
salts; usually expressed as a percentage:
(Influent Quality - Product Quality) x lnn
(Influent Quality)
Salt Passage - The percentage of salts passing through the membrane
as compared to the initial pollutant concentration. Equal to 100
minus salt rejection.
157
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BIBLIOGRAPHIC DATA
SHEET
1. Report^No. .
.-670/2-73-100
4. Title and Subtitle
Application of Reverse Osmosis to Acid Mine Drainage
Treatment
3. Recipient's Accession No.
5» Report Date
December, 1973
6.
7. Author(s)
Roger C. Wilmoth
8- Performing Organization Rept.
No.
9. Performing Organization Name and Address
U.S. Environmental Protection Agency
Crown MLna i)rainage Control;Field,Site, Box 555
Rivesville, W. Va. t:26588
10. Prqject/Task/Wprk Unit Nc
lBBOiio/21AFY/31
11. Contract/Grant No.
12. Sponsoring Organization Name and Address
U.S. Environmental Protection Agency
National Environmental Research Center
Cincinnati, OH lj-5268
13. Type of Report & Period
Coveted
Final Report
14.
15. Supplementary Notes
Environmental Protection Agency report number, EPA-670/2-73-100, December 1973.
16. Abstracts Spiral -wound reverse osmosis systems were tested on four different acid mine
drainage discharges in West Virginia and Pennsylvania. Comparison studies were made
of the hollow-fiber, tubular, and spiral-wound systems at a ferrous iron acid discharge;
and of hollow-fiber and spiral-wound systems at a ferric iron acid discharge.
At all sites, the limiting factor in high recovery operation was calcium
sulfate insolubility. An empirical formula was developed for predicting maximum
recovery.
Application of reverse osmosis was demonstrated to be technically feasible
for a large percentage of acid mine drainage discharges.
A process called "neutrolosis" was developed in which the reverse osmosis
brine isneutralized and clarified, and the supernatant recycled to the influent to
the reverse osmosis unit. In this manner, the neutrolosis process discharges only a
high quality product water and a neutralized sludge. Neutrolosis recoveries as high
as 98.8 percent were achieved at a ferric iron acid discharge site.
17. Key Words and Document Analysis. 17a. Descriptors
Acid Mine Drainage*
Reverse Osmosis*
Calcium Sulfate*
Coal Mines
Brine Disposal
Water Pollution Control
Iron
Manganese
17b. Identifiers/Open-Ended Terms
West Virginia*
PennsyIvani a*
Neutrolosis*
Water Recovery
17c. COSATI Field/Group
18. Availability Statement
19.. Security Class (This
Report)
UNCLASSIFIED
20. Security Class (This
Page
UNCLASSIFIED
21- No. of Pages
22. Price
}RM NTIS-35 (REV. 3-72)
-159-
USCOMM-DC 14952-P72
J.S. GOVERNMENT PRINTING OFFICE: 1974 546-516/Z63
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