Environmental Protection Technology Series
INDEPENDENT PHYSICAL-CHEMICAL
     TREATMENT OF  RAW SEWAGE
               Municipal Environmental Research Laboratory
                     Office of Research and Development
                    U.S. Environmental Protection Agency
                            Cincinnati, Ohio 45268

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                                  EPA-600/2-77-137
                                  August 1977
       INDEPENDENT PHYSICAL-CHEMICAL
          TREATMENT OF RAW SEWAGE
                     by

              Leon S. Directo
              Ching-Lin Chen
              Robert P. Miele
  Los Angeles County Sanitation Districts
        Whittier, California  90607
          Contract No. 14-12-150
              Project Officer

             Irwin J. Kugelman
        Wastewater Research Division
Municipal Environmental Research Laboratory
          Cincinnati, Ohio  45268
MUNICIPAL ENVIRONMENTAL RESEARCH LABORATORY
     OFFICE OF RESEARCH AND DEVELOPMENT
    U.S. ENVIRONMENTAL PROTECTION AGENCY
          CINCINNATI, OHIO  45268

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                               DISCLAIMER
This report has been reviewed by the Municipal Environmental Research
Laboratory, U. S. Environmental Protection Agency, and approved for
publication.  Approval does not signify that the contents necessarily
reflect the views and policies of the U. S. Environmental Protection Agency,
nor does mention of trade names or commercial products constitute endorse-
ment or recommendation for use.

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                              FOREWORD
The Environmental Protection Agency was created because of increasing
public and government concern about the dangers of pollution to the health
and welfare of the American people.  Noxious air, foul  water, and spoiled
land are tragic testimony to the deterioration of our natural environment.
The complexity of that environment and the interplay between its components
require a concentrated and integrated attack on the problem.

Research and development is that necessary first step in problem solution
and it involves defining the problems, measuring its impact, and searching
for solutions.  The Municipal Environmental Research Laboratory develops
new and improved technology and systems for the prevention, treatment, and
management of wastewater and solid and hazardous waste  pollutant discharges
from municipal and community sources, for the preservation and treatment of
public drinking water supplies, and to minimize the adverse economic, social
health, and aesthetic effects of pollution.  This publication is one of the
products of that research; a most vital communications  link between the
researcher and the user community.

Independent physical-chemical treatment of municipal wastewater is  an alter-
native technology to biological treatment for achieving secondary effluent
standards.  This report summarizes a successful long-term pilot plant
investigation of one mode of this new concept in wastewater treatment.
                                    Francis T.  Mayo
                                    Director,  Municipal  Environmental
                                      Research  Laboratory

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                                ABSTRACT


     A 3.17 I/sec (50 gpm) pilot plant evaluation of the independent
physical-chemical treatment (IPC) process was conducted for 27 months at
Pomona, California under the auspices of the U.S. Environmental Protection
Agency and the Los Angeles County Sanitation Districts.  The pilot plant
consisted of chemical clarification with alum at 25 mg/1 as Al and an
anionic polymer at 0.3 mg/1 followed by a single-stage, pressurized down-
flow carbon column operated at a hydraulic loading of 2.71  1/sec/m2
(4 gpm/ft2) and an empty-bed contact time of 30 minutes.  The main objectives
of the study were to evaluate various methods of controlling sulfide
generation in the carbon column and to determine the effects of repeated
thermal regeneration cycles on the adsorption capacity, carbon loss,
pressure buildup of IPC carbon.

     Performance data obtained have demonstrated the stability of the IPC
system in producing effluent of excellent overall quality.   The suspended
solids, total COD and total phosphate removals in the IPC system were
96.6%, 94%, and 92%, respectively.

     In the course of the study, several methods of controlling sulfide
generation in the carbon column, such as oxygenation, chlorination, and
sodium nitrate addition, were evaluated.  Of the methods evaluated,
continuous sodium nitrate addition to the carbon column at an average
dosage of 5.4 mg/1 N was found most effective in preventing sulfide
generation.

     The addition of nitrate had another favorable effect in that it permit-
ted, through enhancement of biological activity, a very high organic
loading on the carbon column.  At the end of the first cycle, the carbon
capacity was 3.54 Kg total COD removed/Kg carbon and 1.54 Kg dissolved
COD removed/Kg carbon.

     Although regeneration was not necessary, it was conducted in an effort
to obtain data on the effects of repeated regenerations on the carbon
characteristics.   These were the first large-scale regenerations of granular
activated carbon used in the IPC mode.  In all respects, the regenerations
were as successful as those conducted on granular activated carbon used in
the tertiary treatment mode.  The performance of the regenerated carbon was
found equal to or slightly better than that of the virgin carbon.

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      This report was submitted in fulfillment of Contract No.  14-12-150  by
the Los Angeles County Sanitation Districts,  Whittier,  California  under  spon-
sorship of the U.S.  Environmental Protection  Agency.   This report covers  the
period from January 1973 to August 1975.

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                               CONTENTS


Di s cl a i mer	i i

Foreword   	  i i i

Abstract   	   i v

Figures	 viii

Tables     	    x

Acknowledgements	  xii

      1.   Introduction   	   1

              Background of the  study  	   2

      2.   Conclusions  	   3

      3.   Recommendations 	   6

      4.   Experimental  Program	   7

              Pilot plant description and operation	   7
              Sampling  and testing  program  	  16

      5.   Experimental  Results 	  18

              Chemi cal  treatment phase  	  18
              Carbon treatment phase     	  39
              Carbon regeneration results  	  71
              Discussion of system  performance   	  83

      6.   Economic Analysis	  97

              Chemical  treatment costs  	  97
              Carbon treatment costs    	 102
              IPC  system costs  	 102


References  	105
                                    vi

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                               FIGURES

 Number                                                            Page

 1   Schematic diagram of the IPC pilot plant	  8

 2   Carbon contactor detai1  	 10

 3   Detail of  the  carbon  column  underdrain  system...	 12

 4   Cross sectional view of the multiple hearth furnace 	 13

 5   Schematic diagram of the air pollution  control  system	15

 6   Hourly variation in suspended solids concentration  	 20

 7   Variation in suspended solids concentration and alum dose .... 22

 8   Suspended solids removal patterns in the IPC system -
       first cycle	24

 9   Suspended solids removal patterns in the IPC system -
       second cycle	27

10   Suspended solids removal patterns in the IPC system -
       third cycle  	28

11    Zone settling velocity as a function of suspended solids
       concentration	30

12   Batch flux curves of IPC sludge with and without polymer 	 31

13   Batch flux curve with polymer	32
                                                                   •
14   Effect of cycle time on  filter  yield and cake solids 	34

15    Performance of various chemical conditioning agents
       at 2 minutes  cycle time	35

16    Performance of various chemical conditioning agents
       at 4 minutes  cycle time  	36
                                  vm

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                          FIGURES(CONTINUED)



Number                                                             Page

17   Effect of chemical dosage on filtrate quality 	 37

18   Variation in the carbon effluent total sulfide concentration.. 42

19   Effect of nitrate feed disruption on sulfide production 	 47

20   Surface wash-water backwash schedule  	 50

21   Air-water backwash schedule  	 51

22   Carbon column suspended solids loading and pressure drop -
       first cycle	 53

23   Carbon column suspended solids loading and pressure drop -
       second cycle	 56

24   Carbon column suspended solids loading and pressure drop -
       third cycle	 57

25   COD removal through the carbon column - first cycle 	 59

26   COD removal through the carbon column   second cycle 	 63

27   COD removal through the carbon column - third cycle 	 65

28   Effect of regeneration on DCOD removal capacity 	 67

29   Effect of regeneration on per cent DCOD removal  	 68

30   DCOD profile through the carbon column 	 70

31   Turbidity and color removal through the carbon column -
       first cycle 	 72

32   Turbidity and color removal through the carbon column -
       second cycle 	 75

33   Turbidity and color removal through the carbon column -
       thi rd cycl e 	 76

34   Effect of copper waste on COD removal 	 88

35   Effect of copper waste on suspended solids removal 	 89

36   Effect of copper waste on turbidity removal	 90

37   Proposed IPC system flow sheet 	100
                                   ix

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                               TABLES

Number

 1  Virgin Carbon Characteristics
 2  Summary of Chemical Clarification System Performance
      wi th Ferri c Chi ori de ......................... .
 3  Summary of Chemical Treatment System Performance
      wi th Al urn and Polymer ............... ,
 4  Leaf Filter Test Results ..... .... ...... . ......... . ..... . ..... 38

 5  H2S Control Measures i n the Carbon Col umn ................ .... 40

 6  Performance of the Various H S Control Measures .......... .... 48

 7  Carbon Capacity in IPC Plants ........................... . ____ 69

 8  Carbon Col umn Performance ...... ................... .......... . 77

 9  Effect of Regeneration on the IPC Carbon Characteristics ..... 79

10  Furnace Operating Conditions during IPC Carbon
      Regenerati on .............. . ....... ....... ...... ..... ..... . . 81

11  Summary of Air Pollution Control System Performance ...... .... 84

12  Summary of IPC System Performance  ... ................. . ...... 86

13  Heavy Metal Analyses .................. . ................. . ____ 91
                                                                  *
14  Mineral and Miscellaneous Analyses ... .................... .... 92

15  Heavy Metal Constituents of Quench Water and Carbon Samples  .. 94

16  Nitrogen Removal  in the IPC System .. ____ .... ____ . ....... ..... 95

17  IPC System Design Data  ........ .... .......................... 98

18  Unit Costs for Operation and Maintenance Estimate ---- ........ 99

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                           TABLES(CONTINUED)







Number                                                             Page



19  Estimated Chemical Treatment Costs 	  "101



20  Estimated Granular Activated Carbon Treatment Costs 	  103



21  Estimated IPC System Costs 	  104

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                           ACKNOWLEDGEMENTS
     This project was  undertaken  through  a  cooperative effort of the
Environmental  Protection  Agency and the Los  Angeles  County Sanitation
Districts.   The pilot  plant evaluation was  conducted at the Sanitation
Districts Advanced Waste  Treatment Research  Facility in Pomona,  California.

     Acknowledgement is made to Mr.  Arthur  N.  Masse, Former Chief,  Municipal
Treatment Research Program of the Advanced  Waste  Treatment Research
Laboratory in  Cincinnati, Ohio, for his invaluable  advice  in the planning
stage of the project.   Thanks are also extended to  Mr.  William Lee, Former
Project Engineer of the Sanitation Districts,  for his  participation in the
initial stages of the  pilot plant study.

     The untiring efforts and assistance  of  both  the laboratory  and the pilot
plant operating personnel of the  Pomona Advanced  Waste Treatment Research
Facility are gratefully acknowledged.

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                             SECTION 1

                            INTRODUCTION
      The application of granular activated carbon in wastewater treatment
technology has been greatly explored during the past ten years.  This wide-
spread use of the carbon has been attributed to the successful  development
of economical methods of regenerating the exhausted carbon.   The large-scale
use of granular activated carbon in wastewater treatment, however, has been
primarily confined to the so-called tertiary treatment approach, in which
the carbon treatment phase follows the conventional biological  secondary
treatment.  In this treatment approach, there are inherent benefits achieved:
lower organic load to the carbon bed thus allowing either higher effluent
quality or shorter contact time; lower influent suspended solids, thus
reducing the headless through the carbon bed and obviating problems related
to physical plugging, ash buildup and eventual accelerated loss of the adsorp-
tive capacity of the carbon after repeated thermal regeneration cycles; and
finally, lower supply of bacterial nutrients in the feed to the carbon column,
thus reducing problems associated with abundant biological growth, septicity
and possible hydrogen sulfide generation.

      The other carbon treatment approach which has gained widespread interest
in recent years is the independent physical-chemical  treatment  (IPC) of
municipal and industrial wastewaters, in which chemically clarified raw
sewage or primary effluent, with or without prior inert media filtration,is
applied to the carbon column.  This carbon treatment approach attempts to
maximize the use of the granular activated carbon by including  in its
function not only the removal of refractory dissolved and biodegradable
organic materials but also the use of the column as a deep bed  filter for
the removal of suspended and colloidal solids.  Consequently, the carbon bed
is loaded as heavily as possible within the limits of desired effluent
quality.  The IPC approach thus seeks to supplant conventional  biological
treatment processes.  In this respect, the IPC process inherently offers
several major advantages over conventional biological treatment systems,
namely,  IPC is practically immune to upsets due to materials toxic to
biological systems, such as heavy metals from industrial waste  discharges;
it is more readily adaptable to rapid changes in influent flow  and waste-
water composition;it has lower space requirements; and finally, the IPC
process can remove a significant amount of heavy metals.

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BACKGROUND OF THE STUDY

     In recent years, there have been several  IPC pilot plant studies con-
ducted by various investigators (1,2,3).   Although these studies have
indicated that IPC system can achieve excellent wastewater treatment, none
was conducted for an extended period of time.   Thus,  operational problems
such as sulfide generation, excessive column headless and deterioration of
carbon properties which can only become manifest with time, were not
thoroughly investigated.   In addition, at none of these installations was
carbon regeneration practiced.   While the technology  for carbon regeneration
in a multiple hearth furnace has been well  developed  and demonstrated for
granular activated carbon used  after biological  treatment (tertiary treat-
ment mode), it has not yet been applied for granular  activated carbon used
in the IPC mode.   Therefore, this study was conducted to evaluate the per-
formance over an  extended period of time  of an IPC system which includes
regeneration of the granular activated carbon.

     The specific objectives of the study were:   To evaluate the performance
of the chemical  clarification system using  alum and polymer; to demonstrate
on a long-term basis, the effectiveness of  granular activated carbon in the
removal of soluble organic matter from chemically clarified raw sewage; to
evaluate methods  of controlling hydrogen  sulfide generation in the carbon
column; to determine the  effects of repeated thermal  regenerations on the
carbon characteristics and performance, and finally to develop the cost
estimates for the IPC system.

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                              SECTION 2

                             CONCLUSIONS
     1.  The IPC pilot plant, consisting of a 3.78 I/sec (60 gpm) chemical
clarification system followed by a 3.16 I/sec (50 gpm) single-stage, packed-
bed, down flow granular activated carbon column, was operated successfully
for 27 months.  Extensive operating data collected during the field eval-
uation had demonstrated the capability of the IPC system in consistently
producing effluents of excellent overall quality.  The average carbon
effluent TCOD, DCOD, suspended solids, turbidity and color were 19.3 mg/1 ,
13.5 mg/1, 6.7 mg/1, 6.3 JTU and 7.8, respectively.

     2.  During the virgin adsorption cycle, the carbon capacity was 3.54
Kg TCOD removed/Kg  carbon and 1.54 Kg DCOD removed/Kg carbon.  The corres-
ponding carbon dosage was 0.021 Kg carbon/m3 (173 Ibs carbon/mil, gal).
The DCOD removal efficiency did not change appreciably in the course of the
virgin run, during  which time 113,550 m3 (30 million gallons) of chemically
clarified raw sewage was processed through the column.

     3.  The organic removal through the carbon column during the entire
study averaged 79.9 percent for TCOD, 72.2 percent for the DCOD and 78.5 for
BOD5.  The DCOD removal efficiency through the carbon column increased
following sodium nitrate addition to the carbon column as a result of
enhancement of biological activity.  The DCOD removal efficiency of the
regenerated carbon  was higher than that of the virgin carbon.  The carbon
capacity of the twice-regenerated carbon was slightly less than that of the
once-regenerated carbon.

     4.  Analyses of metals on carbon prior to and after the first regen-
eration indicated that some of the metals which were removed from the sewage
were not removed during regeneration.  However, most of the metals removed
by the carbon did not remain on the carbon but were carried out of the
furnace with the flue gases.  Dust collected from the baghouse contained high
levels of Ca, Cd, Cu, Cr, Al , Fe, Sn, Pb, Ni and Zn.   Some of these came
from corrosion in the carbon column rather than from the sewage.

     5.  An evaluation of the carbon characteristics following repeated
thermal regenerations showed that after three regenerations, the iodine
number and methylene blue number decreased about 26 and 5 percent, respec-
tively.  During the same period, the molasses number increased about 3.6
percent.   The ash content of the carbon increased about 67 percent from

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 a  virgin  level of 6.4 to 10.7 percent after the first regeneration.  On the
 second  regeneration, only a slight increase in ash content was observed
 while a decrease was noted in the third regeneration.

     6.   The  carbon regeneration loss ranged from 2.5 to 6 percent with an
 overall average of 4.3 percent for the three regenerations.

     7.   Of the various methods of sulfide control evaluated-namely, oxygen
 addition,  chlorination, air-water backwash and sodium nitrate addition,
 continuous sodium nitrate addition to the carbon column at an average
 dosage  of 5.4 mg/1 N  was found most effective in inhibiting sulfide
 generation in the carbon column.

     8.   The  level of sodium nitrate required is  a function of the
 organic concentration in the feed to the carbon column.  The level
 required  at Pomona to prevent sulfides is specific for the wastewater, and
 should  not be directly transferred to any other situation.  A rough rule
 of thumb  is that the nitrate should be about 15 percent of the DCOD in
 the  feed  to the carbon column.

     9.   The carbon column, which served both as deep bed filter and an
 adsorber, was routinely backwashed on a daily basis with a volume of
 secondary effluent equivalent to 7 percent of the product water.  The net
 headloss  through the column during the daily backwash cycle varied
 considerably during the study.  The weekly average net headloss varied
 from 0.11  Kg/cm2 (1.6 psi) to 3.1 Kg/cm2  (44 psi).  The net headloss was
 equal to  or less than 1.76 Kg/cm2  (25 psi) 50 percent of the time.

    10.   The bulk of the pollutant removal in the IPC system was accomplish-
 ed during the chemical clarification phase.  Chemical clarification using
 alum at an average dosage of 25 mg/1 Al  (275 mg/1 alum) with 0.3 mg/1 of
 anionic polymer (Calgon WT-3000) was very effective throughout the study
 in producing good quality clarified effluent from raw sewage.  The clar-
 ified effluent had an average turbidity, suspended solids and TCOD
 concentrations of 22.2 JTU, 28.3 mg/1 and 95.8 mg/1, respectively.  The
 total phosphate in the raw sewage, which had averaged 11.1 mg/1 P, was
 reduced by 88 percent, resulting in a clarified effluent with total
 phosphate  concentration of 1.3 mg/1  P.

    11.   Results of bench-scale sludge studies performed in the course of
 the study  showed that the alum-sewage produced was difficult to dewater.
 Chemical conditioning at a cost of $15-$17 per ton dry solids was
 required to achieve a yield of 4.9-9.8 Kg/m2-hr (1-2 Ib/ft2-hr) with
cake solids of 18 percent.

    12.   The total  treatment cost for a 37,850 cu m/day (10 mgd) IPC
system designed to produce a product water with an average TCOD of 25 mg/1,
 DCOD of 16 mg/1  and suspended solids of 8 mg/1 using alum and polymer, is
estimated  at 8.69<£/m2 (32.57(^/1000 gallons).   The estimated cost is based

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on using an 8 x 30 mesh granular activated carbon with carbon dosage of
0.03 Kg/m3 (250 Ib/mil. gal) and a carbon regeneration loss of 5 percent
per cycle.  If regeneration were not required the cost is reduced to
7.92<£/m3 (29.68(^/1000 gallons).  These cost estimates are representative
of price levels as of March 1975, with an EPA sewage treatment plant
construction cost index of 232.1.

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                             SECTION 3

                          RECOMMENDATIONS
      1.  The results of the pilot plant study presented in this report
indicate that the granular activated carbon column performance in the
first adsorption cycle remained virtually unchanged throughout the 18.5
months of operation.   Although not necessary, the column was regenerated
to obtain data on the effects of repeated thermal regenerations on the IPC
carbon column performance.   It is recommended to conduct a long-term eval-
uation of the IPC carbon column without regeneration to determine the ulti-
mate COD removal capacity.

      2.  Further studies should be carried out to determine the mechanism
by which the biological  acitvity on the carbon column allowed significantly
higher carbon capacity.   In this connection, attempts should be made to
determine the cause of the  apparently higher COD removal capacity of the
regenerated carbon compared to virgin carbon.

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                             SECTION 4

                        EXPERIMENTAL PROGRAM
PILOT PLANT DESCRIPTION AND OPERATION

      Figure 1 shows the process flow sheet of the IPC pilot plant.  The
pilot plant consisted of a 3.78 I/sec (60 gpm) chemical clarification system
followed by a 3.15  I/sec (50 gpm) single-stage, packed-bed, granular
activated carbon column operated in downflow mode.  A carbon regeneration
facility complete with an air pollution control system was available in the
pilot plant site.   The details of the design and operation of the various
components of the pilot plant are discussed in subsequent sections.

Chemical Treatment  System

      The chemical  treatment system consisted of a rapid mixing unit 0.76m
square  (2.5 ft. square) with 1.07m (3.5 ft.) liquid depth followed by a
three-compartment flocculation unit 1.37m (4.5 ft.) wide and 4.11m (13.5 ft.)
long with 1.67m (5.5 ft.) liquid depth equipped with three variable speed
paddle-type flocculators.  The raw sewage was pumped at a constant rate of
3.78 I/sec (60 gpm) into a rectangular stilling tank provided with a V-notch
weir for flow measurement.  The chemical coagulant, either alum or ferric
chloride, was fed directly to the rapid mixing unit by means of three timer-
controlled positive displacement chemical pumps paced in such a way as to
approximately match the incoming suspended solids concentration.  The
diurnal variations  of the raw sewage suspended solids concentration was
previously established by the analysis of hourly samples collected over
several 24 hour periods.  This feeding pattern was periodically checked
during the course of the study by routinely analyzing for suspended solids,
six four-hour composite samples of raw sewage and clarified effluent. An
anionic polymer (Calgon WT-3000) was added as a coagulant aid at an average
dosage of 0.3 mg/1.  The polymer addition was confined to only 12 hours per
day, from 11  a.m.  to 11 p.m.  to coincide with the period of high coagulant
dosage.  After 2.8 minutes of rapid mixing at 140 rpm, the sewage flowed
into the flocculation unit where slow stirring for 42.5 minutes theoretical
detention time was provided.   The flocculation was operated at a velocity
gradient, G of about 54 seconds"1.   The G value was obtained by calculation
assuming a drag coefficient of 1.5 and a water velocity equal to 3/4 of the
radial  velocity at the center of the wooden paddles.   The G value for rapid
mixing was not estimated since an auxiliary air mixing was also used.

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RAPID        FLQCCULATION
 MIX
    POLYMER
                                              SEDIMENTATION
      ALUM.
        OR
      FeCk
   SEWAGE
co
ADSORPTION


  NdN03
1
I 1 ! I I
J C
n r
i i i » i
-
^*-SLUDGE
                                                                     CARBON
                                                                     RETURN
                                                                               TO REGENERATION
                                                                              *~ FACILITIES
                                                                               PRODUCT
          Figure !. Schematic diagram of the  IPC  pilot plant.

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     The chemically coagulated raw sewage flowed into a rectangular clar-
ifier where it was settled for a theoretical detention time of 84 minutes.
At the flow rate of 3.78 I/sec (60 gpm)5 the clarifier overflow rate and
weir rate, were respectively, 48 cu m/day/m2 (1180 gpd/ft2) and  2.06
1/sec/m  (10 gpm/ft).   The clarified effluent flowed by gravity to a 1.89-
cu m (500-gallon) surge tank from which 3.15 I/sec (50 gpm) was pumped
continuously to the carbon column.  The clarified effluent tank was
provided with an overflow and a low level cut-off switch for pump protection
The chemical sludge was pumped continuously from the clarifier sludge
hopper at a constant rate of 0.17 I/sec (2.8 gpm) during the first 14
months of the study.  Thereafter, the chemical  sludge pump operation was
placed on a timer control to withdraw sludge at 0.17 I/sec (2.8 gpm) for
15 minutes every hour.  The intermittent sludge withdrawal was initiated
in an effort to obtain more concentrated sludge.

Carbon Treatment System

     The carbon column, shown in detail in Figure 2, was 1.22m (4 ft) dia-
meter  by 9.45m (31 ft) high and was designed for a working pressure of
3.52 Kg/cm2 (50 psi).   The interior of the column was coated with three
coats of 8 mills each of Koppers Bitumastic 300 M coal tar epoxy to inhibit
corrosion.  The column contained 2360 Kg (5200 Ibs.) of Calgon Filtrasorb
300 (8 x 30 mesh granular activated carbon) having virgin characteristics
shown in Table 1.  The 4.87m (16 ft) deep carbon bed was supported by
20.32 cm (8 in) layer of graded gravel placed over Leopold filter blocks.
Figure 3 shows the detail of the column underdrain system.

     The chemically clarified raw sewage entered the top of the column
through a 10.16 cm (4 in) pvc pipe.  Throughout the study, the column was
operated in a downflow mode at a constant flow rate of 3.15 I/sec (50 gpm)
thereby providing a hydraulic loading of 2.71 1/sec/m2 (4 gpm/ft2) and an
empty-bed contact time of 30 minutes.  The column influent discharge outlet
was located about 3.66m (12 ft) above the top of the carbon bed, thereby
providing a capability of as much as 75 percent bed expansion during back-
washing.  The column was provided with rotary surface wash mechanism
mounted about 7.62 cm (3 in) above the unexpended carbon bed to aid in the
routine column backwashing.

Carbon Regeneration System

     The carbon regeneration facility at the pilot plant site consisted of
a 7 6 cm (30 in) internal diameter vertical refractory-lined Bartlett-
Snow-Pacific, Inc. multiple hearth furnace.  As illustrated in Figure 4,
the furnace contained six hearths with two gas burners and steam inlets
in each of the lower three hearths.  The furnace was natural gas-fired with
steam added to enhance the regeneration.

     The partially dewatered spent carbon from the drain bin was fed by
a screw conveyor provided with a variable speed drive so that the desired

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       II" X 12"
       PORTHOLE
INFLUENT
BACKWASH
         WASH
        WATER*
oo
evi
    <£>
ro
   EFFLUENT-*-,
   BACKWASH-
                  CARBON BED SURFACE
                          4ft.
                                         REGENERATED CARBON
                                         CHARGE
                                        ROTARY SURFACE SPRAY
                                             2ft.  MANHOLE
                                         CARBON DISCHARGE
                                        -UNDERDRAIN SYSTEM
                                               I =2.54 cm.
         Figure 2.  Carbon contactor  detail.
                            10

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TABLE 1.   VIRGIN CARBON CHARACTERISTICS
Carbon Characteristics
Iodine Number ,
Apparent Density ,
Molasses Number
Methyl ene Blue Number,
Ash , %
Mean Particle Diameter
Sieve Analysis :
% retained on #








mg/g
3
g/cm

mg/g

, mm
8
10
12
14
16
18
20
30
pan
Calgon Filtrasorb 300
(8 x 30 mesh)
1040
0.484
222
256
6.4
1.44
3.5
12.6
19.2
16.3
15.1
9.0
6.8
11.7
5.8
                     11

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   LEOPOLD —
  FILTER BLOCK
                                                            '••'."2" LAYER  '/Q-  10 MESH '.'.

                                                                       LAYER '4" -'/8"
                                                                                    cm
                                                                 CARBON EFFLUENT
                                                                    LINE
Figure 3. Detail of the carbon column underdrain system.

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           CARBON IN
                               GAS OUT
     6'-0
DRY CARBON
SAMPLING
SHAFT
DRIVE
UNIT
                                         RABBLE
                                           ARM
                                         RABBLE
                                         TEETH
                                         3-0 DIAMETER
                                            1"= 2.54 cm
                                       REGENERATED
                                       CARBON OUT
                                              TO QUENCH
                                                 TANK
Figure 4. Cross sectional view of the multiple hearth furnace.
                           13

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rate of carbon  fed to  the  furnace  could  be  accurately controlled.   The
regenerated carbon was discharged  from the  furnace  through a 7.62  cm (3 in.)
diameter stainless steel  chute  leading from the  bottom hearth into a quench
tank, from which the regenerated,  quenched  carbon was continuously educted
back to the carbon contactor.

Air Pollution Control  System

     In order to control  noxious odors and  particulate emissions,  which are
the two major air pollutants associated  with thermal  regeneration  of
granular activated carbon, the  regeneration furnace was equipped with an
air pollution control  system shown schematically in Figure 5.  The air
pollution control system consisted of a  single  cyclone dust separator, a
baghouse, and a natural  gas-fired  afterburner.   During carbon regeneration,
the furnace flue gases first passed through the  cyclone, which was designed
to trap all burning particulates 10p in  diameter or larger before  reaching
the fabric filters in  the baghouse.   From the cyclone, the gases flowed
through a series of ducts into  a baghouse.   The  ductwork leading to the
baghouse was provided with a valved connection  for  dilution air addition.
The baghouse was a reversed-air jet cleaned unit (Model 9-6-100 Mikro-
Pulsaire Dust Collector manufactured by  Mikropul  Division of Slick Corpor-
ation) containing nine 11.43 cm (4.5 in.) diameter  Nomex felt filter bags
with a combined filter area of  5.94 sq.  m (64 sq.ft.).  Each filter bag
was 1.83m (6 ft.) long and was  designed  for a maximum operating temperature
of 218.3°C (425°F).  The filter bags had a  rated porosity of 0.17  to 0.99
cu m/min. (25 to 35 scfm)  at 1.27  cm '(0.5 in.)  water column.  The  dust-laden
flue gases flowing at a rate ranging from 3.96  to 4.53 cu m/min (140 to 160
scfm) entered the lower section of the baghouse  and travelled upward through
the fabric filter cylinder where the dust particles collected on the
exterior surface of the filter  bags.  A  pull-through exhaust fan mounted
on top of the baghouse provided the driving force for the gas flow through
the system.  As the dust mat built up on the fabric surface, the pressure
differential across the filters increased to a  level  at which the  deposited
solids had to be removed by reverse air  flow.  In order to control the
pressure drop through  the filter within  the desired limits of 2.54 cm (1 in.)
to 15.24 cm (6 in.) of water column, a cyclic timer periodically (2 to 45
seconds interval) actuated solenoid valves  which delivered momentary
surges of compressed air rated  at  7.03 Kg/cm  (100  psi).  The dust dislodged
from the exterior surface of the filters during  the reverse jet cleaning
operation were collected in a storage drum  attached to the discharge "hopper
of the baghouse.  The  filtered  gases from the baghouse then flowed through
the afterburner which  was  operated between  704.4°C  (1300°F) and 760°C (1400°
F) for odor control before final discharge  into  the atmosphere.
                                     14

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c_n
                             TO
                         ATMOSPHERE
                FUEL


                  AIR
                                  AFTERBURNER
                                                           BLOWER
     SPENT CARBON IN-

      MULTIPLE
        HEARTH
                             FLUE GAS
  FURNACE

       STEAM-
        FUEL-
COMBUSTION AIR-
                                     CYCLONE
                     REGENERATED
                     CARBON OUT
                                DUST TO
                              STORAGE DRUM
     QUENCH
      TANK
      TO
     CARBON
     COLUMN
                 MAKE-UP WATER
                 MOTIVE WATER
                                                               «—-COMPRESSED AIR FOR
                                                                   PULSED AIR
                                                                   CLEANING OF BAGS

                                                                BAGHOUSE
  DUST TO
STORAGE DRUM
            EDUCTOR
     Figure 5. Schematic  diagram of the  air pollution control system.

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 Carbon Transfer and Regeneration Procedures

      Prior to each regeneration the spent carbon was backwashed with 56.8
 m3  (15,000 gallons) of secondary effluent from the main Pomona plant and
 hydraulically transferred to the dewatering bin.  The dewatered spent
 carbon, with about 50 percent moisture content, was conveyed through a
 screw conveyor into a six-hearth furnace where it was regenerated at
 temperatures ranging from 899°C (1650°F) to 977°C (1790°F).  Steam in the
 amount of 0.6'Kg steam/Kg carbon was added to the lower two hearths to
 enhance regeneration.  The regenerated carbon was discharged from the
 furnace at the rate of 35-41 Kg/hr (77 to 90 Ibs/hr) into a quench tank
 from  which it was continuously educted back into the carbon contactor.  The
 regeneration of one batch of spent carbon normally required 53-66 hours to
 complete.  After regeneration, the regenerated, quenched carbon was back-
 washed with 75.7 m3 (20,000 gallons) of secondary effluent to remove the
 carbon fines and the appropriate amount of virgin make-up carbon was added
 to  replace the carbon lost during the regeneration.  The weight of the
 virgin carbon added to make up to the original volume was used as the
 measure of the carbon loss.  The column, with the added make-up carbon, was
 then  given a final backwash of 7.57 m  (2000 gallons) of secondary effluent
 before it was placed back in operation.

 SAMPLING AND TESTING PROGRAM

      In this study, samples of raw sewage, chemically clarified raw sewage
 and carbon effluent were obtained 5 days a week using specially designed
 automatic samplers programmed to collect six 4-hour composite samples a
 day.  Each 4-hour composite was made from samples collected automatically
 for 3 to 5 seconds once every 15 minutes.  For sewage sampling, a Sirco
 automatic sampler was used in conjunction with the aforementioned sampling
 devices.   The 4-hour composite sampl.es were manually combined to obtain
 a 24-hour composite sample.  All samples taken were refrigerated at 4 °C
 prior to analysis.  The 24-hour composite samples were analyzed daily for
 total chemical oxygen demand (TCOD), dissolved chemical oxygen demand (DCOD),
 turbidity, suspended solids and color; two to three times a week for
 alkalinity, ammonia, nitrite, nitrate, total aluminum and total phosphate;
 once  a week for total  dissolved solids, sulfate, organic nitrogen, methylene
 blue-active substances; and once to twice a month for phenols, minerals
 and metal  constituents.   About three times a week, the six 4-hour composite
 samples were individually analyzed for COD and suspended solids in order to
monitor more closely the diurnal variations of these parameters.  Tests for
pH, temperature,  dissolved oxygen (D.O.) and total sulfides were performed
 three to  five times a week on grab samples.  Grab samples of chemical sludge
were analyzed daily for suspended and volatile solids., and one to two times
a week for total  phosphate and total aluminum.  Periodically during the study,
thickening and filtration tests were performed on sludge samples.
                                      16

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     Occasionally, 24-hour composite samples from various depths of the
carbon column were collected using timer-controlled solenoid valves.
These samples were analyzed for DCOD to determine the movement of the
soluble organics wavefront through the carbon column.

Analytical Methods

     All physical and chemical analyses were performed in accordance with
the 13th Edition of Standard Methods (4) or the FWPCA Methods for Chemical
Analysis (5) unless otherwise specified.

     The mineral and metal analyses were performed using atomic adsorption
methods.  Dissolved oxygen was determined by the use of Weston and Stack
dissolved oxygen analyzer.  Turbidity was determined by the use of a
Rossum turbidimeter.  Tests for ammonia, nitrite, and nitrate were performed
using a Technicon Auto-Analyzer.  The activated carbon analyses were
performed using  standardized procedures (6).

     The thickening tests were performed using 2-liter graduated cylinders
each fitted with a picket rake mechanism operated at a rotational speed
of  1 revolution  per minute (rpm).
                                                                    r\
  2  The leaf  filtration tests were conducted using a standard 93 cm  (0.1
ft   ) Eimco  leaf filter under a vacuum of 38cm (15 in.) of mercury.  Two-
liter samples  of gravity-thickened and chemically-conditioned sludge were
used in the  filtration tests.

Regeneration Schedule

     When the  carbon became exhausted based on a predetermined level of
either effluent  quality or organic loading, the column was taken off stream
in  preparation  for regeneration.  In this study, the original criterion
for  regeneration was a carbon effluent total chemical oxygen demand (TCOD)
limit of 40  mg/1.  During the virgin adsorption cycle, however, it was
found that  the  carbon effluent TCOD concentration remained practically
constant at  a  level of about 20-24 mg/1 through the first 18 months of
column operation.  Because of this observation, it was decided to dis-
regard the  effluent TCOD criterion and to regenerate the carbon.  Thus,
in  the second  and third adsorption cycles, the carbon was regenerated
every 3 to  5 months without regard to the state of exhaustion of the
carbon in an effort to obtain data on the effect of repeated thermal re-
generations  on  the carbon characteristics and performance.  The data
generated in this study was divided into three groups to correspond to the
carbon column  operation in between the regenerations.
                                     17

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                             SECTION 5

                        EXPERIMENTAL RESULTS
 CHEMICAL TREATMENT PHASE

 Performance

     During the first one and one half months of the study when the carbon
 column was being installed, ferric chloride, which was available from a
 previous study was used for coagulation.   After this shakedown operating
 period, ferric chloride was replaced with alum as the primary coagulant.
 Table 2 presents the performance of the chemical treatment system with
 ferric chloride addition.  The raw sewage TCOD and suspended solids con-
 centration during the ferric chloride addition period was about 50 percent
 higher than that observed during the major portion of the study when alum
 was used as the coagulant.  Because of the high influent TCOD and suspended
 solids concentration, the corresponding clarified effluent concentrations
 were also high.  When expressed as percent removal, however, the TCOD and
 suspended solids removal with ferric chloride were comparable to those
 observed with alum addition.

     Starting in March 1972, when the carbon column was placed in operation
 until  the termination of the study, alum, at an average dosage  of 25 mg/1
 Al (275 mg/1  alum) was used as the primary coagulant in the chemical treat-
ment of the raw sewage.  During the first month of alum addition, solids-
 liquid separation in the sedimentation tank was rather poor, resulting in
excessive amounts of floe being carried over with the clarified effluent.
 In order to enhance settling of the alum floe, an anionic polymer (Calgon
WT-3000) was  added at an average dosage of 0.3 mg/1 to the first compart-
ment of the flocculation unit.  While alum was fed continuously, the
polymer was added for only 12 hours per day corresponding to the period of
high alum dose.  As mentioned previously, the alum feeding was varied through-
out the 24-hour period to approximately match the influent suspended solids
 concentration.  In order to check the effectiveness of the pacing of the
 alum feed, hourly samples of raw sewage and clarified effluent collected over
 several 24-hour periods were analyzed for suspended solids.  The results of
one of these  tests are shown in Figure 6.  These hourly suspended solids data
 clearly demonstrate the effectiveness of the chemical clarification system
 in producing  consistent effluent quality.  Periodically, during the course
 of the study, the effectiveness of the dosing pattern was checked by
                                      18

-------
TABLE 2.   SUMMARY OF CHEMICAL CLARIFICATION SYSTEM PERFORMANCE WITH FERRIC CHLORIDE
Ferric Chloride
Dosage, mg/1
Fed 3
80
107
Raw Sewage, mg/1
TCOD
495
483
Susp.
Solids
280
303
Total
P
11.4
12.7
Clarified Effluent (mg/1)
TCOD
160
136
Susp.
Solids
52
52
Total
P
2.1
1.8
% Removal
TCOD
67.9
71.8
Susp.
Solids
81.4
82.8
Total
P
81.6
85.8

-------
    320
    280
    240
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  05
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  ID
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    120
  C/5
     80
    40
               AVG.
'W-RAW SEWAGE

         A  .
                                      ALUM. DOSE =24 mg/l AI3+

                                      POLYMER DOSE = 0.3 mg/l
\
                   \
      /   V
      /

                              ^
                                            /,
                                                      \     /
                          •CLARIFIED EFFLUENT
                                  I
      7A.M.
       3PM.
                   7

                 TIME
3A.M.
Figure  6. Hourly  variation in  suspended  solids  concentration.
                               20

-------
routinely analyzing for suspended solids the six 4-hour composite samples
of raw sewage and clarified effluent.  Typical results of the analysis of
the six 4-hour composite samples for suspended solids, which are presented
in Figure 7, indicate that the pacing of the chemical dosage was indeed
effective in producing chemically clarified effluent of essentially constant
quality.  Figure 7 was prepared by plotting the average of 17 days data for
the month of July, 1972.  Data for other months also show similar perform-
ances.

     Table 3 presents a summary of the average performance of the chemical
treatment system during the course of alum addition.  The system perform-
ance during each of the three periods corresponding to the three adsorption
cycles of the granular activated carbon column is shown separately in the
table.  As indicated in the table, the overall suspended solids and TCOD
removal efficiencies in the chemical clarification phase were 85.8 percent
and 70.2 percent, respectively.  Throughout the study, the chemical treat-
ment system was highly effective and consistent not only in the removal of
suspended solids and TCOD, but also in the removal of total phosphate.  The
chemically clarified effluent had an average TCOD of 95.8 mg/1  and an average
suspended solids of 28.3 mg/1.  The dissolved COD concentration, however,
remained virtually unchanged during the chemical  treatment.  This observa-
tion is contrary to what other investigators have found (3,12).  The average
total phosphate concentration in the raw sewage was reduced from 11.1 to 1.3
mg/1 P during the alum treatment.  Additional removal of suspended phosphate
was achieved through the carbon column thereby boosting the overall total
phosphate removal efficiency through the IPC  system to 91.9 percent.

     Figures 8 through 10 illustrate the weekly average suspended solids
removal patterns.  The data in these figures along with those presented in
Table 3, demonstrate that with the exception of the DCOD removal, the major
portion of pollutant removal was accomplished in  the chemical treatment
system.  Moreover, it is apparent from the data that in spite of the consid-
erable variation in the raw sewage strength, the  chemical  clarification
system performance remained relatively stable.
Sludge Thickening and Dewatering Properties
     During the first fourteen months of the study, the sludge produced in
the chemical clarification system was withdrawn continuously at the rate of
0.17 I/sec (2.8 gpm) without any attempt to thicken the sludge.  Because of
this continuous sludge withdrawal the sludge produced was rather dilute
with an average suspended solids concentration of only 4100 mg/1 (ranged
from 1700 to 6500 mg/1).  From the 15th  month  until  the  termination
of the study, the sludge pumping operation was placed in an intermittent
mode in an attempt to further thicken the sludge in the sedimentation tank.
The total daily sludge volume withdrawn amounted to about 1.2% of pilot
plant flow.  The suspended solids concentration of the sludge varied from
about 1 to 2% during the period when intermittent sludge withdrawal was
practiced.  The sludge contained 1.6 percent total phosphate and 8.3 percent
total  aluminum on a dry solids weight basis.
                                     21

-------
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280


240

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CO I2°
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40


i— 	 r 	 T 	 • 	 1 	 s i
1 " 1
1 AVG. ALUM. DOSE = 24 mg/l AI3 +
j POLYMER DOSE =0.3 mg/l
_ ,_J | RAW SEWAGE;
1
~~ j^-4-HR. COMPOSITE
1 ^ 24- HR. COMPOSITE -
1
1
_ —

1 	
I

_ —
j 	 .__
ALUM. DOSE^



CLARIFIED EFFLUENT"-
^r4-HR. COMPOSITE
^24-HR. COMPOSITE
111 i


















30
20

10


7A.M. II 3RM. 7 II 3A.M. 7
TIME
                                                                u
                                                                CO
                                                                o
                                                                o
Figure 7. Variation in  suspended  solids  concentration  and alum

          dose.
                                22

-------
        TABLE 3.    SUMMARY OF CHEMICAL TREATMENT SYSTEM PERFORMANCE WITH ALUM AND POLYMER^
Parameters
Suspended Solids, mg/1
Turbidity, JTU
TCOD, mg/1
DCOD, mg/1
BOD5, mg/1
Color
Total Phosphate, mg/1 P
Nitrate, mg/1 N
pH
Raw Sewage
(a)
205

331
50.4


11.3

7.65
(b)
180

295
45.6


11.1

7.67
(c)
198

315
50.8


9.6

7.78
Overall
Avq.
199

3?1
49.4


11.1

7.68
Clarified Effluent
(a)
30.9
24.4
9R 4
48
38.8
19.2
1.5
0.92
6.85
(b)
22.8
19.9
86.2
48.4
30.4
20.4
0.86
.87
6.64
(c)
24.5
20.6
98.2
52.1
33.6
21.6
0.85
.78
6.40
Overall
AVQ.
28.3
22.9
95.8
48.6
36.2
20
1.3
.90
6.75
Percent Removal
(a)
84.9

70.3
4.8


86.7


(b)
87.3

70.8



92.3


(c)
87.6

68.8
...


91.1


Overall
Avg
85.8

70.2
1.6


88.3


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    *   Average  alum dosage = 25 mg/1  Al  (275  mg/1  alum);  Average  polymer  dosage  =  0.3 mg/1  Calgon  WT-3000
    (a)   1st  cycle  average concentration
    (b)   2nd  cycle  average concentration
    (c)   3rd  cycle  average concentration

-------
4="
             350
                                        VOLUME TREATED, million gallons
                                          5.5        7.3      8.8       10.3
                                           12        16        20
                                        STUDY PERIOD,  (WEEKS)
12.6
                                                             UNIT CONVERSIONS
                                                             mil gal x 3785 = cu m
                                        RAW SEWAGE
                                           CLARIFIED EFFLUENT
                             CARBON EFFLUENT
          Figure 8- Suspended  solids removal pattern  in the  IPC system- first cycle

-------
  350
     12.6
14.4
    VOLUME TREATED, million gallons
15.9      16.6      18.0       19.6
21.5
23.1
24.8
    32
                                                     UNIT CONVERSIONS:
                                                     mil gal x 3785 = cu m
                            CLARIFIED EFFLUENT
          40
          44       48        52
       STUDY  PERIOD, (WEEKS)
 56
 60
 64
Figure 8. Continued

-------
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          VOLUME TREATED, million gallons
      24.8     25.6     28.6      30.0
   300
£  250
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                                                  UNIT CONVERSIONS:
                                                  mil gal x 3785= cu m
                          RAW SEWAGE
                CLARIFIED EFFLUENT
                                  CARBON EFFLUENT
     64
              68
72       76       80       84
        STUDY PERIOD, (WEEKS)
88
92
96
 Figure 8. Continued

-------
  350
               1.8
VOLUME TREATED, million gallons
   3.7       5.5        7.3       9.1
10.3
                                  CLARIFIED EFFLUENT
                             CARBON EFFLUENT
                                                   T
                                                 UNIT CONVERSIONS:
                                                 mil gal x 3785= cu m
                                                                             /*>
                                 12        16       20
                               STUDY PERIOD, (WEEKS)

Figure 9. Suspended  solids removal patterns in the  IPC  system-second cycle.

-------
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            300
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                 VOLUME TREATED, million gallons
                        1.8       3.4       5.1
                                             RAW SEWAGE
                                                           UNIT CONVERSIONS:
                                                           mil gal x 3785 - cu m
                                  CLARIFIED EFFLUENT
                                             CARBON EFFLUENT
                                  8       12        16       20

                                         STUDY PERIOD, (WEEKS)
                                                           24
28
32
           FigurelO. Suspended  solids  removal  patterns in the  IPC  system-third cycle.

-------
     In the course of the study, a limited number of batch settling tests
were performed on grab sludge samples using two-liter graduated cylinders,
each fitted with a picket rake mechanism.  The picket rakes were operated
at^a constant rotational speed of one revolution per minute to reduce wall
effects on sludge compaction in the graduated cylinders and thus approximate
to a certain degree the settling phenomenon observed in a full-scale
thickener.  The batch settling tests were performed using various levels of
initial suspended solids concentrations with and without the use of polymers
as thickening agents.  From the sludge settling curves obtained, zone
settling velocities were calculated by taking the slope of the initial
straight line portion of the settling profile.  Figure 11 shows a log-
arithmic plot, of the zone settling velocity as a function of the initial
suspended solids concentration.  The beneficial effect of polymer on the
settling properties of the IPC sludge is shown by comparison of the curves
in Figure 11.  Figures 12 and 13 present solid flux curves, which were
derived by calculation using the zone settling velocity-suspended solids
concentration data in Figure 11.  These batch flux curves are useful in
evaluating a number of alternate thicker design by selecting various
possible underflow concentrations.  Operating lines drawn tangent to the
batch flux plot provide the maximum solids flux through the thickener at the
desired underflow concentration.  For instance, as indicated in Figure 12,
for an underflow concentration of 4 percent solids the maximum solids flux
was 61 Kg/nr/day (12.5 lbs/ft"/day) for a sludge without polymer and 156.2
Kg/nf/day (32 lbs/ft-/day) for sludge thickened with 4.22 Kg/t (9.3 Ibs/ton
dry solids) of Dow Chemical C-41 polymer.  As indicated in Figure 13, the
corresponding solids flux for sludge thickened with 0.82 Kg/t (1.82 Ibs/ton
dry^solids) of American Cyanamid polymer 905 N was 597.8 Kg/nr/day (122 Ibs
/ft2/day).  While the solids flux data obtained have indicated a significant
reduction in the thickener size with the use of polymer as a thickening
agent, an economic analysis should be performed in order to determine whether
the polymer use is justified.

     Several leaf filtration tests were performed using various types of
polymers for chemical conditioning.  The conditioning agents were evaluated
at various cycle times to derive optimum filter performance based on
filter yield, cake solids and filtrate quality.  The sludge samples were
first concentrated to about 2 percent suspended solids concentration by
gravity-thickening for a period ranging from 16 to 18 hours.  The filter
tests were performed using a standard 93 cnf (0.1 ft2) Eimco leaf filter
under a vacuum of 38  cm (15 in.) of mercury.  For each test run, a 2-liter
sample of the chemically-conditioned sludge was used.  A monofilament
nylon 415 was used as the filter medium in all the leaf filter tests.

     The two most important variables -controlling directly the economics of
sludge dewatering by vacuum filtration are the chemical  dosage and the
filter yield.  Moreover, the ultimate sludge disposal cost is influenced
directly by the moisture content of the filter cake produced during the sludge
dewatering operation.  In an attempt to evaluate the relationships of the
                                      29

-------
   10

   8
O
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>  1.0

1   8
ui   6
CO
ui

I   4
             IPC SLUDGE
        UNIT CONVERSIONS^
        ft/hr x 0.305 = m/hr.
        Ibs/ton x 0.5= kg/metric ton
        TEMPERATURE	22°-23
        O	O WITHOUT POLYMER
        £* -A WITH DOW CHEMICAL
             POLYMER C-41 (9.3 Ibs.
        O	O WITH AMERICAN CYANAMID
             POLYMER 905N (1.82 Ibs
                                 /TON)
                     34      6   8  1.0         2     34
                     SUSPENDED SOLIDS CONCENTRATION, %
Figure II.  Zone  settling  velocity as a function of suspended solids
          concentration.
                               30

-------
   40
   35
   30
   25
I  20

 •»
X
c/>   15
O
o
en
    10
       IPC SLUDGE

TEMPERATURE	22°-23°C
0—0 WITHOUT  POLYMER
      WITH DOW CHEMICAL
      POLYMER  C-41 (9.3lbs/TON)
                               UNIT CONVERSIONS:
Ibs/ton x 0.5= kg/metric ton
Ibs/ft2/day x4.9= kg/mVday
       O
                       I
                                             OPERATING
                                               LINES
                    I
                       2345
                SUSPENDED SOLIDS CONCENTRATION, %
Figure 12.  Batch flux curves of IPC sludge with and without
           polymer.
                             31

-------
                                   IPC SLUDGE
                            TEMPERATURE	23° C
                            POLYMER DOSAGE— 1.82 Ibs/Ton
                            TYPE OF POLYMER---AMERICAN
                                              CYANAMID 905N
                            UNIT CONVERSIONS:
                            Ibs/ton x 0.5= kg/metric ton
                            Ibs/ftVday x 4.9= kg/mVday
             OPERATING
               LINE
                       2345

                 SUSPENDED  SOLIDS CONCENTRATION, %
Figure  13. Batch flux curve of IPC  sludge with polymer.
                            32

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aforementioned  variables,  leaf  filter  tests were  performed using various
types  of  polymers  at  different  dosage  levels  and  under  three different
cycle  times.  The  test  results  showed  that the  filter yield increased
with increasing chemical dosage and  that  the  greatest yield increase
occurred  at  the 2-minute cycle  time.   Moreover, in comparing the data for
different cycle times.,  it  is  shown that while the lower cycle time pro-
vided  relatively higher filter  yield,  it  also provided  a wetter cake.  Thus,
in plant  scale  dewatering  operation, a judicious  choice of cycle time and
chemical  dosage should  be  made  in such a  way  as to achieve an optimum
combination  of  filter yield and cake moisture.  Figure  14 summarizes the
effect of cycle time  on both  filter yield and cake solids.

     The  results of a second  series  of leaf filtration  tests, in which
ferric chloride along with six  different  types of polymers were evaluated
at various dosage  levels and  cycle times, are summarized in Figures 15, 16
and 17.   The  parameters used  to evaluate  the  performance of the various
chemical  conditioning agents  were filter  yield, percent cake solids and
filtrate  suspended solids  concentration.  To  facilitate the comparison of
the performance of the  various  conditioning chemicals,  the results are
presented in  terms of the  chemical cost expressed in $/ton dry solids.

     Figure  15  shows  the effect of chemical dosage at 2-minute cycle time
on the filter yield and cake  solids.   The corresponding data for the 4-
minute cycle  time  is  presented  in Figure  16.  As indicated by the trend of
the curves in Figures 15 and  16, the filter yield increased with increasing
chemical  dosage up to an optimum dosage level, beyond which, the yield
decreased with  further  increase  in the dosage.  Moreover, it is evident
from the  curves that  although higher chemical dosage provided higher
filter yield, it also resulted  in a wetter cake.  The effect of chemical
dosage on  filtrate quality is shown  in Figure 17.   In comparing the perform-
ance of the  various chemical  conditioning agents,  as shown in Figures 15  and
16, it is  apparent that under the laboratory test condition, the Dow
Chemical  C-31 showed  the best performance based on filter yield and percent
cake solids.  However,  as  depicted in  Figure 17, the filtrate contained a
high concentration of suspended  solids.   All the other polymers evaluated
produced  a clear filtrate  at  the higher dosage levels.   Ferric chloride at
a dosage  level  as high  as  12.3  percent by weight of sludge solids was not
found  effective for IPC sludge  conditioning.

     Table 4  summarizes the leaf filter test results in which ferric chlo-
ride and  various types  of  polymers were used as chemical conditioning agents.
The data  in the table were obtained from  the plot presented in Figure 16.
The last  two  columns  of Table 4  show the  filter yield and the corresponding
conditioning  chemical cost to obtain 18 percent cake solids.   The test
results indicated  that alum-sewage sludge with initial solids concentration
of 1.61 to 2.26 percent were  dewatered to 18 percent cake solids with yields
ranging from  2.4 to 5.4 Kg dry  solids/hr/m2(0.5 to 1.1   Ibs.dry solids/hr/sq
ft of  filter  area).   Of the chemicals  evaluated, the Dow chemical anionic
polymer A-23  appeared to be the most effective in  terms of chemical cost,
yield, cake solids, and filtrate quality.   Moreover, it is of interest to
                                     33

-------
   25
   20
 CO
 9

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 CO
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 X.
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    10
I  3
M-
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tri
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               I         23         4         5

         O—O CALGON WT. 2640 (73.4 Ibs./TON DRY SOLIDS)

              DOW CHEMICAL C-41 (93 Ibs./TON DRY SOLIDS)

              AM. CYANAMID 905N (0.54 Ibs./TON DRY SOLIDS)


                                 UNIT CONVERSIONS:
                                 Ibs/ton x 0.5= kg/metric ton
                                 lbs/ft*/hr x 4.9= kg/mVhr
     0
                        234
                           CYCLE TIME,min.
Figure 14. Effect of cycle time on  filter  yield and cake solids.
                                34

-------
               25
CO
en
                                             SUSP SOLIDS CONC.-»-l.85% TO 2.26% (IPC SLUDGE)
                                             FILTER MEDIA -»> NYLON 415
                                             CYCLE TIME-*2 MIN.ftO SECS.FORM TIME 8 80 SECS.
                                                              DRY TIME)
                                             VACUUM-*38.1 cm Hg
                                             n-OCALGON E207
                                              -0 FERRIC CHLORIDE
                                                 CALGON WT. 2640
                                                 AM. CYANAMID 905 N
                                             O-O DOW CHEMICAL C-31
                                             O—o DOW CHEMICAL C-41
                                                 I	I	i
UNIT CONVERSIONS:
Ibs/ftVhr x4.9=kg/ma/hr
                                 10
40
                  50
                             15      20      25      30      35

                             CHEMICAL COST, $ /TON DRY SOLIDS

Figure 15. Performance of various chemical conditioning agents at 2 min. cycle time.

-------
GO
en
               25
               20
             
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             UJ
             5 !0
              £ 0
             £  2

             Q"
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                      \
      CALGON WT. 2640
      FERRIC CHLORIDE
  a-QCALGON E207
  A-AAM. CYANAMID 905 N
  0—0 DOW CHEMICAL C-41
-O-ODOW CHEMICAL C-31
  •--•DOW CHEMICAL A-23
                                             UNIT CONVERSIONS:
                                             lbs/ft«/hr x4.9=kg/m*/hr

                                   SUSP. SOLIDS CONC.-»-l.85% TO 2.26%(IPC SLUDGQ
                                   FILTER MEDIA-* NYLON 415
                                   CYCLE TIME-*4MIN.(IMIN. FORM TIME 8 3 MIN. DRY
                                                    TIME)       ,        1A
                                 10
40
                                                                      50
                               15      20      25      30      35
                            CHEMICAL  COST, I/TON DRY SOLIDS
Figure 16. Performance of various  chemical conditioning  agents at 4 min. cycle time.

-------
           12,000 f
CO
                                       SUSPENDED SOLIDS CONC.-* 1.85% to 2.26% (IPC SLUDGE)
                                       FILTER MEDIA— NYLON 415
                                       CYCLE TIME-* 2 MINUTES (40 SECS.FORM TIME AND
                                                              80 SECS. DRY TIME)
                                       VACUUM-^38.1 cm Hg
                                                    O— O
                                                    A--A
      CALGON WT 2640
      DOW CHEMICAL C-41
      AM. CYANAMID 905 N
      FERRIC CHLORIDE
      CALGON E-207
O— O DOW CHEMICAL C-31
 «--• DOW CHEMICAL A-23
                                                    D--D
                 0        5        10        15       20       25       30
                                        CHEMICAL COST, VTON DRY SOLIDS

        Figure 17. The  effect of chemical dosage on  filtrate quality.
r                                                                        CLEAR FILTRATE
                                                                        (SUSP. SOLIDS 4-
                                                                         I00mg/l)
                                                                       . --- , - .
                            35
40

-------
                                     TABLE 4.    LEAF FILTER TEST RESULTS
Feed Solids,
Percent
by weight
1.91
2.26
2.15
2.05
1.80
1.61
2.04
1.86
Conditioning
Chemicals
Used
Calgon WT-2640
Calgon E-207
Dow Chemical
C-41
Dow Chemical
C-31
Dow Chemical
A-23
Am- Cyan amid
905 N
Ferric Chloride
None
Chemical
Cost
$/Kg
0.59
0.46
0.17
0.68
3.85
3.74
0.13
0
Based on Optimum Yield
Yield, 2
Kg/hr-m
4.9
5.4
6.4
6.4
10.8
5.4
3.9
2.3
Cake Solids
%
18.5
17.5
12.5
20.0
11.5
13.0
22.5
21.0
Cost,
$/ton
15
20
14
21.5
15
20
8
0
Based on 18% Cake Solids
Yield, 2
Kg/hr-m
4.9
4.4
3.9
-
5.4
2.4
-
-
Cost,
$/ton
15
15
5.5
-
2
6
-
-
CO
co
     *  Filter media used was Nylon 415  (Eimco).   Cycle  time was  4  minutes,

-------
note that at 18 percent cake solids, the filter yield with the use of
American Cyanamid 905  N was  about  the  same  as  that with unconditioned
sludge.  As previously discussed .although the  filter yield increased with
increasing  chemical  dosage,  the resulting filter cakes were found to
contain higher moisture content except  in those runs where ferric chloride,
Dow C-31 and Calgon  WT-2640 were used.

CARBON TREATMENT PHASE

Sulfide Control Measures

     The high concentration  of soluble  organics applied to the carbon
column are  known to  stimulate prolific  biological growths within the column.
Although this biological activity  enhances  the overall carbon capacity
for dissolved organics removal (7), severe  operational problems frequently
occur, such as clogging of the carbon bed and the development of ana-
erobic conditions with the attendant sulfide generation problem.  Pressure
buildup and sulfide  generation were two major operational problems encounter-
ed in the IPC carbon column  operation.

     In the biological oxidation of organic matter various hydrogen acceptors,
either organic or inorganic, are reduced.   As indicated in the literature
(8,9), microorganisms  tend to utilize various hydrogen acceptors
preferentially in the  order:  molecular oxygen, nitrate, sulfate and oxidized
organics.   In the absence of dissolved oxygen and/or nitrate,  sulfate-re-
ducing bacteria depend on sulfate  reduction as a mode of anaerobic energy-
yielding metabolism with hydrogen  sulfide as one of the reduced by-products.
For sulfate reduction  to take place, the following conditions  have to be
satisfied:  presence of organic matter and  sulfates; absence of dissolved
oxygen and/or nitrate  and an environment with favorable temperature.  The
biological  slimes and  deposits provide favorable sites where the microbial
environment becomes  suitable for hydrogen sulfide generation.   Thus, in
the use of  columnar  granular activated carbon beds for filtration-adsorption
of chemically clarified raw sewage, the potential  for production of
hydrogen sulfide is high due to the accumulation of suspended  solids and
other materials providing a large  biomass with a correspondingly high oxygen
demand.  For this reason, efficient surface washing and backwashing
techniques must be employed not only to prevent excessive pressure buildup
but also to minimize solids accumulation on the surface of the bed that
could trigger sulfide generation.

     During the first adsorption cycle, the carbon column was  operated con-
tinuously for two weeks before hydrogen sulfide was first detected in the
column effluent.   In an effort to  inhibit sulfide production,  various
control measures were evaluated with varying degrees of effectiveness as
indicated by the summary data in Table 5 and in Figure 18.  In the first
two months of the column operation, the bed was routinely cleaned by sur-
face wash-backwash procedure, as discussed in detail  in the following
section.   During that period, the  total sulfide concentration  of the column
ranged from 1.0 to 5.7 rng/1  S, and averaged 2.9 mg/1  S.  Because of this
                                      39

-------
       TABLE 5.  H S CONTROL MEASURES IN THE CARBON COLUMN
Control Measures
            Remarks
(a)  Surface wash - water backwash

(b)  (a) + 02 addition to carbon
     column to D.O. level 4 mg/1
     intermittently (4 hrs/day).

     (a) + Continuous 02 addition
     to the carbon column to D.O.
     level of 4 mg/1.

(c)  Surface wash and air/water
     backwash techniques.
(d)  (c)  + aeration of the
     chemically clarified
     effluent to D.O.  level
     2-6 mg/1.
of
(e)   (d)  + 20 mg/1  Cl2 added to
     carbon influent.

(f)   (d)  + 40 mg/1  Cl2 added to
     carbon influent.
(g)   (d)  + NaNO? addition to
     carbon influent at 2.9
     mg/1.
            Sulfides formed.

            A reduction in sulfide formation was
            observed.
            A reduction in sulfide formation was
            observed.  Excessive pressure drop
            occurred in the carbon column.

            During the first few days of air/water
            backwash operation, about 17.8 cm of
            carbon was lost to the underdrain pre-
            sumably due to the disturbance of the
            gravel layer.   The bed cleansing
            efficiency of this technique was not
            significantly better than that of (a).
            A slight reduction in sulfide
            formation was  observed.

            Observed results were essentially the
            same as (b).
            Observed sulfide level in the carbon
            effluent slightly lower.

            Significant reduction in the^sulfide
            concentration was observed.  In
            addition, column headloss was signifi-
            cantly lower than previously observed.

            The continuous addition of sodium
            nitrate, which is preferentially
            reduced during the anaerobic process
            had been the most effective in
            eliminating sulfides.
                                      40

-------
                         TABLE 5 (continued)
Control  Measures
Remarks
(h,i)  (d) + NaNO, addition to
       carbon influent at 4.5-
       5.1 mg/1.

 (j)   (a) + NaN03 addition to
       carbon influent at 5.4
       mg/1.
Complete elimination of sulfide.
Complete elimination  of sulfide.
                                      41

-------
ro
STUDY PERIOD, wt^ks

               81 **3
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                                                                         16
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STUDY PERIOD, weeks

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         AUGUST
   SEPTEMBE
    OCTOBER

       1972
Figure  18.  Continued

-------
                  STUDY PERIOD, weeks
4
6




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MARCH
Figure  18. Continued

-------
high carbon effluent sulfide  level, oxygen was added to the carbon column
in order to prevent sulfate reduction.  Although the carbon effluent sulfide
level decreased slightly, this procedure was abandoned because of excess-
ively high headloss which occurred in the carbon column as a result of
increased biological activity.

     Since sulfate-reducing microorganisms tend to concentrate on biological
slimes and deposits, it follows that an effective bed backwashing would
help in controlling sulfide formation.  Consequently, an auxiliary air
scour was used in conjunction with the surface wash-water backwash procedure.
The expected benefit of the air-water backwash technique, however, was not
achieved.  To some extent this may be because the underdrain of this column
was not basically designed to function with air scour.  Even the oxygenation
of the chemically clarified effluent to dissolved oxygen level  of 2-6 mg/1
in conjunction with the air-water backwash technique did not produce a
significant decrease in the carbon effluent sulfide level.

     In view of this, another control measure, that of continuous chlorine
addition to the carbon influent at dosages ranging from 20 to 50 mg/1  Cl,
was evaluated.  While chlorination of the carbon influent effected some
reduction in the total sulfide formed, the results obtained were not at all
encouraging because of the high dosage required.  Even at a chlorine dosage
as high as 50 mg/1 Cl, sulfide was still present in the carbon  effluent.
In addition, although the average total sulfide concentration in the carbon
effluent during the high chlorine dosage was only 1,13 mg/1  S,  at no time
during the 21 days of continuous chlorine addition, was the sulfide main-
tained at a consistently low level.  The sulfide concentration  in fact
fluctuated throughout the period from .09 to 2.6 mg/1  S as indicated in
Figure 18.  It is of interest to note that during periods of chlorine
addition, especially at the higher dosage of 40-50 mg/1 C], headlosses
through the carbon column were consistently low in spite of the relatively
high influent suspended solids.  This observation demonstrates  that the
high pressure drop observed prior to chlorination and after chlorine
addition ceased, were indeed caused by abundant biological growths in the
carbon column.  Subsequent experience further confirmed the above obser-
vation in that drastic increase in headloss occurred when chlorination
was interrupted for only a few hours.

     In using chlorine for sulfide control in carbon columns, it must be
recognized that activated carbon is an effective dechlorination medium.
Results of chlorine residual determination of samples obtained at various
depths in the carbon column have indicated the complete removal of chlorine
at the top 38.1 cm  (15 in.) of the carbon bed.  The average total chlorine
residual in the liquid just above the carbon surface was about 20 mg/1.
Since the chlorine was completely removed at the top layers of the carbon col
umn, the viable sulfate-reducing organisms remained virtually unchecked in
the lower carbon layers.  Unless the sulfate-reducing organisms are complete-
ly inhibited throughout the column depth, erratic sulfide inhibition would
result as experienced in this study.
                                      45

-------
     Because chlorination at a dosage up to 50 mg/1 was neither completely
effective in eliminating sulfide formation, sodium nitrate addition to the
carbon column was initiated.  During the first month of nitrate addition,
the nitrate dosage was varied from 1.8 to 3.8 mg/l N.  As anticipated, the
nitrate was almost completely removed in the carbon column by biological
denitrification.  The reduction of nitrate in the carbon column was accom-
panied by high headless through the bed.  The total sulfide concentration
of the carbon effluent averaged only 0.36 mg/l S, which was appreciably
less than that obtained with chlorination and other methods previously
evaluated.  From the second to the 7th month of sodium nitrate addition,
the nitrate dosage was maintained in the range of 4.5 - 5.4 mg/l N.
Thereafter, the nitrate dosage was maintained at an average level  of 5.4
mg/l N.  The continuous addition of nitrate to the carbon column influent
at the dosage of 5.4 mg/l N was found very effective in inhibiting the
hydrogen sulfide generation in the carbon column.  Figure 18 shows the
weekly average total sulfide concentration in the carbon effluent.  As
shown in the figure, the total sulfide concentration remained consistently
at zero level.  On a number of occasions, however, nitrate feeding to the
carbon column was disrupted due to a malfunction of the chemical feed pump.
As a result of the cessation of the sodium nitrate feed, sulfide generation
in the carbon column started immediately as indicated in Figure 18 by the
increase in the carbon effluent sulfide concentration during the middle of
October and in the last week of November 1972.  Once the sulfate-reducing
organisms were established in the column, it took several days of contin-
uous nitrate feeding before sulfide generation was fully controlled.
Figure 19 shows detail on the periods when nitrate feed failed.  Thus, the
data obtained during the periods of unintentional interruption of sodium
nitrate feeding proved valuable in demonstrating the need for continuous
nitrate feeding to achieve sustained control of hydrogen sulfide generation.
A comparative performance of the various hydrogen sulfide control  measures
is shown in Table 6.

     In the second and third adsorption cycles, nitrate addition was  not
started until after the first two weeks of operation when sulfides appear-
ed in the column effluent.  The sulfide level was virtually zero in the
column effluent throughout the second and third cycles, except for occasion-
al periods when malfunction of sodium nitrate feed pump occurred.

Column Headloss Data

     Since the granular activated carbon column was operated in a packed-
bed, down flow mode, the column served as a deep bed filter and as an
adsorber.  Thus, the direct application to the column of chemically clar-
ified effluent which contained suspended solids ranging from 25^40 mg/l led
to progressive clogging of the bed with an attendant increase in headloss.
In addition, bacterial growth in the bed played a significant role in the
development of bed pressure drop.  To maintain proper column operation, the
column was backwashed on a daily basis with a volume of secondary effluent
                                     46

-------
                                               SODIUM NITRATE FEED
                                               PUMP MALFUNCTION
       0
                               10          15
                                  TIME, DAYS
Figure 19. Effect of nitrate feed disruption on sulfide production.

-------
           TABLE  6.    PERFORMANCE OF THE VARIOUS H S CONTROL MEASURES
MS Control Measures
(1) Surface wash-backwashing technique
(2) (1) + intermittent 02 addition to
carbon column at D.O. level =
4 mg/1
(3) Surface wash + air/water backwash
plus oxygenation of the chemically
clarified effluent to D.O. 2-6 mg/1
(4) No. (3)+ 20 mg/1 C12* added to
carbon influent
(5) No. (3)+ 40 mg/1 C12 added to
carbon influent
(6) No. (3)+ 2.9 mg/1 N+ added to
carbon influent
(7) No. (3)+ 4.5 mg/1 N
(8) No. (3)+ 5.1 mg/1 N
(9) No.(l)+ 5.3 mg/1 N
(10) No.(l)+ 5.4 mg/1 N
Carbon Effluent Total Sulfide
Cone. , mg/1 S
Average
2.86

1.85
1.87
1.74
1.13
0.3
0.13
0.05
0.019
0
Range
1.0 - 5.7

1.4 - 2.5
0.8 - 3.0
0 - 4.3
0.09- 2,6
0 - 0.95
0 - 0.60
0 - 0.26
0 -*0.10
0 - 0.05
*  Added as sodium hypochloride  solution.
+  Added as sodium nitrate  solution.
                                    48

-------
equivalent to 6 to 8 percent of the product water.  During the course of
the study a number of carbon bed cleaning procedures were evaluated.  The
actual backwash duration varied from 30 to 60 minutes depending on the
procedure used.  Initially, a surface wash-water backwash procedure was
used.  After the column was on stream for several days, with the routine
daily surface wash-water backwash bed cleaning procedure, it was found that
at the end of 24 hours of column operation, the water drained very slowly
from the carbon column.  Thus, during the first adsorption cycle, which
covered the first 18 months of the study, the rotary surface spray was used
without draining the carbon bed.  At the end of the first adsorption cycle
an auxiliary drain line was installed in the carbon column which made it
possible to drain the water in the column to about 38 cm (15 in.) above
the carbon bed before initiating the surface wash cycle.  This auxiliary
drain line was used starting with the second adsorption cycle until  the
completion of the study.

     Figure 20 shows the surface wash-water backwash schedule.  During back-
washing the backwash water was discharged into a holding tank designed to
capture any accidental carbon spills and to allow visual observation of the
clarity of the backwash water.  The  backwash water containing chemical-bio-
logical floe and some carbon fines overflowed a weir in a holding tank and
was pumped into the head end of the primary clarifiers of the Pomona acti-
vated sludge plant.

     For a period of about six months during the first adsorption cycle, an
auxiliary air scour was used in conjunction with the regular surface wash-
water backwash method in an attempt to achieve better bed cleaning and to
provide a means of controlling sulfide generation.   Figure 21 shows  the
air-water backwash schedule.  The air was injected directly into the back-
wash line.  The air-water backwash procedure was found to be only slightly
more effective than the regular surface wash-water backwash procedure.   It
should be pointed out, however, that the column, which was provided  with
the Leopold filter blocks underdrain system, was not designed for air injec-
tion and this could have accounted for the performance observed with the
air scour method.  The loss of about 87 Kg (191  Ibs) of carbon through the
underdrain system during the first few days of the air-water backwash
operation demonstrated that the column underdrain system was not suited for
air injection.  This carbon loss probably occurred when the sudden surge
of air disturbed the graded gravel layers.

     The effectiveness of the various backwash procedures is shown by the
observed column headloss just after backwash and also by the rate of
subsequent headloss buildup.  The headloss just after cleaning was found to
be essentially the same irrespective of the bed cleaning procedure used.
The daily headloss buildup, however, fluctuated considerably during  the
course of the study.  A regression analysis of the  net headloss (headloss
before the daily backwash minus headloss after backwash) and the column
influent suspended solids showed no correlation between the two variables.
This lack of correlation suggests that the major portion of the headloss
                                     49                           u.s. bPA

-------

30
CM
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°- 20
C9
BACKWASH RATE,
D 0

-


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-


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1 1

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WATER=l6.7cu m
UNIT CONVERSIONS:
gpm/ft*x0.68=l/sec/m* -
1 1
                                             15
                                      TIME, MINUTES
20
25
30
35
Figure 20, Surface  wash-water backwash schedule.

-------
4O
30

O
o
CO
2 «


r\
20 U 30
                                   TIME, MINUTES
Figure 21.   Air-water  backwash schedule.

-------
was  due  to biological growths within the carbon-bed which were not  complete-
ly removed during  the routine backwash.  The variations in the weekly average
net  headloss and influent suspended solids concentration are presented  in
Figure 22 for  the  first cycle, Figure 23 for the second cycle and Figure 24
for  the  third  cycle.  As indicated in Figure 22, the pressure losses through
the  carbon column  were very low, ranging from 0.11 to 0.25 Kg/cm2 (1.6  to
3.6  psi), during the first four weeks (week No. 1 to 4  of column operation).
On two other occasions, weeks 11 and 45, the pressure losses were also  low
following a period when the column was out of service for extended  periods
for  repairs.   Moreover, relatively low headlosses, ranging from 0.56 to
1.38 Kg/cm2 (7.0 to 19.6 psi), were observed during the period (weeks 13 to
23)  when chlorine  was added to the carbon column influent for sulfide control.
However, with  the  termination of chlorine addition and the subsequent use
of sodium nitrate  for sulfide control, generally higher headlosses were
observed.  On  several occasions, pressure losses exceeding 3.5 Kg/cm2 (50
psi)  before the daily backwash cycle were recorded.  As indicated previously,
these high pressure losses were probably due to biological solids which
accumulated on and near the top layers of the carbon bed.  These excessive
pressure losses were similar to those observed in previous studies at
Pomona(lO) when granular activated carbon columns were used for denitrifi-
cation purposes.

      As shown in  Figure 24, the headlosses during the first three weeks of
the  third adsorption cycle were also low and exhibited about the same as
that  in the first  adsorption cycle.  In the second cycle, however, the
headloss which is  shown in Figure 23 were high during the first two weeks
following carbon regeneration.  These observed high headlosses were
probably due to carbon fines which were not completely removed in the
initial extended backwash following the carbon regeneration.   In subsequent
periods, weeks No.  3 to 7, the headloss ranged from  0.2 to 0.62 Kg/cnr
(2.8 to 8.8 psi) and showed about the same headloss pattern as in the first
and  third adsorption cycles.

      In a two-day period in December, 1972, about 27.94 cm (11  in.) of
carbon depth equivalent to 136 Kg (300 Ibs) carbon was lost from the carbon
column.  This appreciable amount of carbon loss, coupled with the observed
high headloss at the top 38.1  cm (15 in.) of the carbon bed prompted an
examination of the routine backwash procedure.   It was found that the flow
through surface spray line, which normally was about 0.82 I/sec (13 gpm) with
the  valve fully opened, increased to about 3.16 I/sec (50 gpm).   Th*s ob-
servation led to the examination of the column interior.   It was then
discovered that  the entire rotary surface spray assembly including its
supply pipe was dislodged from its support and buried in the carbon bed.
Accordingly, the column was taken out of service and the carbon, after a
thorough backwash,  was hydraulically transferred to an empty carbon column
in order to retrieve the surface spray assembly.  The rotary spray assembly
was  found intact whereas the 3.81 cm (1  1/2 in.) diameter supply line
(schedule 40,304 stainless steel  pipe) was sheared at two locations.  The
shear failures occurred at the threaded connections where the pipe thickness
                                     52

-------
   80
05

§60

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             2.7
                  VOLUME TREATED, million gallons
                      4.7        6.4       8.8
        10.6
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                                   UNIT CONVERSIONS:
                                   mil gal x 3785= cu m
                                   psi x 0.0703 = kg/cm2
                       10        15       20

                       STUDY PERIOD,  (WEEKS)
                                                  25
                 30
Figure 22. Carbon column  suspended solids  loading and
          pressure  drop- first cycle.
                              53

-------
 _ 80
              14.0
VOLUME TREATED, million gallons

   153       16.6       18.3
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                                        z E o
                                    FLOCCULATOR DOWN
                                   «*-
                                    FOR REPAIRS
     30
35       40       45        50

       STUDY PERIOD, (WEEKS)
55
                                         60
Figure 22. Continued
                                54

-------
\  80
CO
      VOLUME TREATED, million gallons
             25.2      274      29.7
Q
LJ
Q
  60
CO
OL
                                   UNIT CONVERSIONS:
                                   mil gal x 3785= cu m
                                   psi x 0.0703 = kg/cm*
                       I
                   I
    60
65       70       75       80
       STUDY PERIOD  (WEEKS)
85
90
Figure 22. Continued.
                             55

-------
  80
CO

Ii 60
O
CO
             2.1
Q
UJ
Q
2
UJ
Q_
CO
Z>
CO
40
UJ
ID
   20
   60
CO
Q_

CO
CO
O
  40
UJ
X
  20
                VOLUME TREATED, million gallons
                    4.5       6.9	9.1    S0.3
               —T        I         I      1
                                    UNIT CONVERSIONS:
                                    mil gal x 3785 = cu m
                                    psi x 0.0703 = kg/cm*
                       10        15       20
                     STUDY PERIOD  (WEEKS)
                                                25
30
                 column suspended solids  loading and
         pressure  drop— second  cycle.
                              56

-------
_ 80
\
 CP
 E

co"

9

d60
CO

Q
UJ
Q
  40
CO
Z>
CO
UJ 20
Z)
_J
Li.
   60
CO
Q_


CO
CO
O
  40
UJ
X
        VOLUME TREATED, million gallons

             2.2       4.3    5.5
I
T
T   I
                       UNIT CONVERSIONS:
                       mil galx 3785scu m
                       psi x 0.0703= kg/cm*
                                        JL
                      10       15       20

                     STUDY PERIOD, (WEEKS)
                                   25
                                    30
Figure 24. Carbon column suspended  solids loading and
          pressure drop— third cycle.
                              57

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was considerably less than the nominal wall thickness of 3.18 mm (1/8 in.).
The supply line was replaced with thicker walled 3 04 stainless steel
schedule 80 pipe and welded socket fittings were used to connect the rotary
spray assembly to the supply line.  In addition, a 5.08 cm x 5.08 cm x 0.64
cm (2 in. x 2 in. x 1/4 in.) angle iron coated with bitumastic coal tar
epoxy was welded to the supply line for support.

     During the three-week period (Dec. 27, 1972 to Jan. 17, 1973)  when the
column was off stream, the graded gravel  layers over the Leopold blocks were
removed to examine the underdrain system.   The gravel layers were completely
intermixed with carbon, probably due to the use of the auxiliary air scour
during routine backwash.   In examining the Leopold blocks, it was found that
at two locations in the underdrain system the grout was dislodged leaving a
gap of 3.18 to 6.35 mm (1/8 to 1/4 in.) wide by about 15.24 cm (6 in.) long
between the filter blocks and the tank interior.  The sudden surge  of air
during the air-water backwash procedure could have caused the dislodgement
of the grout.  Possibly,  some carbon losses occurred through these  openings
and some losses also occurred during the backwash since carbon was  found in
the backwash water scavenger tank.  The openings between the filter block
anH the tank interior were refilled with grout and a new 20.32 cm (8 in.)
 uy'ei  of graded gravel was placed over the filter blocks.   When the column
operation resumed on Jan. 17, 1973, the use of the air scour was terminated
and the surface wash-water backwash procedure was adopted until the comple-
tion of the study.   In all subsequent periods, no sizeable carbon loss was
observed.

Organic Removal and Effluent Quality

     The major function of the carbon treatment step is the removal  of
soluble organic material  from the chemically clarified raw sewage.   In
addition, substantial  removal of organic suspended solids  was expected as
the packed bed of carbon  served as a filter. In evaluating the column per-
formance, the COD test was used as the primary parameter.   The COD  removal
patterns for the three adsorption cycles  are presented in  Figures 25 through
Figure 27.   It is evident from the figures that the column removed  a major
portion of the influent COD both suspended and soluble.

     The COD removal through the carbon column during the  virgin adsorption
cycle is presented in  Figure 25.  As the COD breakthrough  curves show, the
organic removal through the carbon column  was excellent and remaine*d practi-
cally constant throughout the entire cycle.  The column treated 113,550 m3
(30 million gallons) of chemically clarified raw sewage before it was taken
out of service for regeneration.  It should be pointed out, however, that at
the time the column was taken off-stream for regeneration, the carbon was
still  far from exhausted3 based on the original regeneration criterion of
an effluent TCOD of 40 mg/1.  The decision to regenerate the carbon was
based entirely on the  need to obtain data  on the effect of repeated thermal
regenerations on the carbon performance and characteristics.  In subsequent
adsorption cycles,  the column was regenerated after 3 to 5 months run with-
                                     58

-------
en
i-D
            150
            125
            100
           0
           8
             50
             25
                 UNIT CONVERSIONS'
                 mil gal x 3785 = cu m
                                _L
                                          STUDY PERIOD, weeks
                                                  8
                 13
                                                             CARBON INFLUENT TCOD
           ARSON INFLUENT DCOD
I
CARBON EFFLUENT DCOD
   	I	
                                246
                                VOLUME TREATED,  MILLION GALLONS
                           18
                                                           ARBON EFFLUENT TCOD
          Figure 25. COD removal through the  carbon  column-  first cycle.

-------
cr>
O
            150
            125 -
            100 -
o>
£

Q"
O
O
                                         STUDY PERIOD, weeks
                                                30
                                                         CARBON INFLUENT TCOD
       UNIT CONVERSIONS:
       mil gal x 3785= cu m
                                                     CARBON  INFLUENT DCOD
                                                   /CARBON EFFLUENT TCOD

                                                                      -JH
                                                         CARBON EFFLUENT DCOD
                                                                   I
                                10                12                14

                                 VOLUME TREATED,  MILLION GALLONS
         Figure 25. Continued

-------
en
            150
              40
            125
            100
o>
E 75
 e»
O
O
O
             50
             25
                   ,-o
               16
                      48
STUDY PERIOD, weeks
       53
57
62
           Figure 25. Continued
                                                                   II
                                      CARBON INFLUENT TCOD
                                                        UNIT CONVERSIONS:
                                                        mil gal x 3785= cu m
                                    CARBON INFLUENT DCOD
                                            CAR80N EFFLUENT TCOD
                                           \CARBON EFFLUENT DCOD
                                          	\	
                       18                20                22
                              VOLUME TREATED, million gallons
                                          24

-------
CTl
IX)
              62
            125
            100
E  75

o~
O
O
            50
            25
              24
                      STUDY PERIOD, weeks
                      67              71
76
                                1
                                                    UNIT CONVERSIONS:
                                                    mil gal x 3785 =cu m
                                   CARBON INFLUENT TCOD
                                   CARBON ^FLUENT DCOD
                                                  CARBON EFFLUENT TCOD
                                    'CARBON EFFLUENT DCOD
                                         	I	
                                                         I
                     26                28                30
                          VOLUME TREATED, million gallons
                  32
          Figure 25. Continued

-------
CO
            150
            125
            100
             75
Q

O
O
             50
             25
               0
                                           STUDY PERIOD, weeks
                                                    9
                        UNIT CONVERSIONS:
                                                         13
                                                        CARBON INFLUENT TCOD
                                   EFFLUENT DCOD
                                             .CARBON EFFLUENT TCOD

                                                  *             «v
                                                            •*.-*•.--o>»<
                      246

                        VOLUME TREATED,  million  gallons
17
                                                   CARBON INFLUENT DCOD
 8
          Figure 26. COD  removal through the carbon  column - second  cycle.

-------
  150
        STUDY PERIOD, weeks
        18             22
  125
  100
Q
O
O
   75
   50
   25
                                                         T
                                           UNIT CONVERSIONS:
                                           mil gal x 3785 = cu m
                             CARBON  INFLUENT TCOD
      CARBON  INFLUENT DCOD
I
                            CARBON EFFLUENT TCOD
                            CARBON EFFLUENT DCOD
                            	I	
                      10                12                14
                         VOLUME TREATED, million gallons
                                                    16
Figure 26.Continued

-------
CTv
cn
             150
             125
             100
           o»
           E
Q
O
O
           r 75
             50
             25
                 STUDY PERIOD, weeks
                        5             9
                                                              13
                                                TT
                                          CARBON INFLUENT TCOD
                                                    T    V
                                                               UNIT CONVERSIONS:
                                                               mil gal x 3785 = cu m
            ,CARBON EFFLUENT DCOD
 CARBON INFLUENT DCOD


        rCARBON EFFLUENT TCOD



J         	    I
               0246
                                  VOLUME TREATED, million gallons

           Figure 27 COD  removal through the carbon column—third cycle.
                                                                          8

-------
out any regard to the state of exhaustion of the carbon.  Based on  the  total
throughput volume of 113,550 m3 (30 million gallons) the carbon capacity
during the virgin cycle was 3.5 kg TCOD removed/kg carbon and 1.54  kg DCOD
removed/kg carbon.  The corresponding carbon dosage was 0.021 kg carbon/m3
(173 Ibs carbon/mg).

      The effect of repeated thermal regenerations on the DCOD removal
capacity at various levels  of DCOD applied is presented in Figure  28.  As
shown by the curves, the DCOD removal capacity of the twice-regenerated
carbon is predictably slightly less than that of the once-regenerated carbon.
Moreover, it is also apparent from the curves that the regenerated  carbon
performance was unexpectedly much better than that of the virgin carbon.
The observed higher DCOD removal capacity of the regenerated carbon during
the second and third adsorption cycles could be ascribed to enhanced bio-
logical activity resulting from continuous sodium nitrate addition  to the
carbon column.  It should be pointed out that during the virgin adsorption
cycle, sodium nitrate was not added to the carbon column until after 0.8 kg
DCOD/kg carbon was applied to the column.   As Figure 28 shows, in subsequent
periods following the nitrate addition, the DCOD removal capacity of the
virgin carbon improved significantly to such a degree as to parallel the
DCOD removal curves for the regenerated carbon.  Figure 29 shows a  plot of
DCOD removal in each cycle as a function of DCOD applied.  The data clearly
show the improved organic removal performance during the second and third
adsorption cycles and the favorable effect of nitrate addition on virgin
carbon.  These observations have significant economic impact in that con-
tinuous sodium nitrate addition to the column for sulfide control also
enhanced the biological  activity within the column, thereby increasing the
apparent COD removal capacity of the carbon.  With increased carbon
capacity for organic removal, the carbon column could be operated for extend-
ed periods of times without regeneration and still  maintain practically con-
stant effluent quality.   This was successfully demonstrated during  the virgin
adsorption cycle when the column effluent COD remained virtually unchanged
through 113,550 m3 (30 million gallons) of throughput volume.  Thus, with
higher carbon capacity or lower carbon  dosage, the regeneration cost, both
for initial  capital investment and operation cost,  would be proportionately
lower.

      For purposes of comparison, carbon capacity and TCOD removal   data from
other IPC pilot plants are presented in Table 7 along with the first adsorp-
tion cycle data from the Pomona study.  The data clearly show the unusually
high carbon  capacity obtained at Pomona.  As previously discussed,  this high
carbon  capacity has been attributed to the enhanced biological activity with-
in the  column resulting  from continuous sodium nitrate addition.

      Figure 30 presents the DCOD removal  profile through the carbon column
at eight different cumulative throughput volumes during the virgin  cycle.
These wavefront data show that about 50 percent of the soluble organic
material  in  the chemically clarified raw sewage was removed during  the first
                                      66

-------
        1.5
CP,
     o
     OQ
     o:
     <
     o
        1-0
     Q
     bJ


     O
     CL

     Q

     8
     Q
ONCE-REGENERATED CARBON
                            START NITRATE ADDITION
                                •TWICE REGENERATED CARBON
                                                             VIRGIN CARBON
          0
                               1.0               1.5

                           DCOD APPLIED, kg/kg CARBON
2.0
2.5
      Figure 28.Effect  of  regeneration on DCOD  removal  capacity.

-------
01
oo
           100
            90
            80
          UJ
          sr

          o
          O 70
          o
          Q
          UJ
          o

          S60
          a.
            50
                                         •IV-
                                                ONCE-REGENERATED CARBON
TWICE-REGENERATED CARBON
               START N09 ADDITION
                                               JL
                      I
                     0.2      0.4      0.6      0.8      1.0       1.2

                                      DCOD APPLIED,  kg/kg CARBON
                                       1.4
        T
2.2      2.4
        Figure 29. Effect of regeneration on percent DCOD  removal.

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                       TABLE  7.    CARBON CAPACITY IN IPC PLANTS
Plants
Lebanon, Ohio
Blue Plains, Washington, D.C.
Ewing - Lawrence, N.J.
Pomona, California
TCOD, mg/1
Influent
67
55
75
98.4
Effluent
27
15
20
23.6
TCOD
Removed,
%
59.7
72.7
73.3
76
Carbon Capacity,
Kg TCOD removed/Kg carbon
0.5
0.7
0.8
3.5
CT)

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    1.0
 LU
 EC

 O
 O
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 Q  .6
 o
 o
 \
 o
    -4
    .2
8.3 MG.
            I3.9TMG.
                                                       UNIT CONVERSIONS:

                                                       mil gal x 3785= cu m
                           10
   15         20         25

CONTACT TIME, MINUTES
             30
35
Figure 30. DCOD profile through the  carbon column.

-------
seven minutes of contact time.  Although the DCOD removal increased with
increasing contact time, it is evident from the curves that the soluble
organics removal did not improve significantly beyond the 19.5 minutes con-
tact time.  Furthermore, the data show that over the 18.5 month period
during which time the carbon processed about 113,550 m3 (30 million gallons)
of chemically clarified raw sewage, the carbon suffered only a slight
decline in performance.

     The turbidity and color removal patterns through the carbon column are
shown in Figures 31 through 33.  As indicated in the figures, both the
carbon effluent turbidity and color remained at low levels throughout the
study.  During the three adsorption cycles, the carbon column removed 72.5
percent of the turbidity and 61 percent of the color, thereby producing an
effluent with an average turbidity of 6.3 JTU and an average color of 7.8.
Table 8 presents a summary of the column performance for each of the three
adsorption cycles.

     These data all indicate a model for the performance of the granular
carbon column in this study.  It is theorized that the granular carbon
column removes all the suspended organics applied through the mechanism of
filtration.  Removal of dissolved organics takes place by a combination of
carbon adsorption and bacterial uptake.  The bacterial metabolism of these
organics both those adsorbed on carbon and those taken up by the bacteria
leads to a demand for a hydrogen acceptor and production of new cells.
These cells and the suspended organics are in effect wasted from the system
during the backwash.  The following calculation indicates that this theory
has some validity.  The average DCOD removal across the carbon column was
35.1 mg/1.  The nitrate used was 5.4 mg/1 as N or 18.5 mg/1 as 0.   Since the
DCOD which is not oxidized is synthesized, the cell production must be 35.1-
18.5 = 16.6 mg/1 as 0 or 16.6/1.42 = 11.7 mg/1 VSS.  Here 1.42 is  the COD
equivalent of the bacterial cell mass.  This produces a sludge yield of
11.7/35.1  or 0.335 mg VSS per mg COD removed.  This value is close to that
reported for the synthesis yield in activated sludge denitrification systems
(15).  It is impossible to expect exact correlation because the SRT in a
carbon column system is unknown.

CARBON REGENERATION RESULTS

Carbon Regeneration Process Control

     The primary goal of carbon regeneration is to restore as much as possible
the exhausted carbon it its virgin properties by effecting maximum removal of
the adsorbed impurities from the pores of the spent carbon with a  minimum
damage to the basic pore structure.  Thus, during regeneration the furnace
operating variables such as temperature, carbon feed rate and steam feed
rate are closely controlled.  Moreover, several laboratory control tests,
such as the tests for apparent density, iodine number and molasses number
are performed in the course of regeneration to monitor the quality of the
regenerated carbon.
                                      71

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             2.
     VOLUME TREATED, million gallons
4.0   ft   5.5       7.3       8.8      10.3
12.6
                                                  i         I
                                    CLARIFIED EFFLUENT
                       CARBON EFFLUENT
                                UNIT CONVERSIONS
                                mil aal x 3785= cu
                              CLARIFIED EFFLUENT
                                                           CARBON EFFLUENT
                                12        16       20
                               STUDY  PERIOD (WEEKS)
Figure 31. Turbidity and color removal through the carbon column-first  cycle.

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CO
              30
                12.6      14.4
               32
36
             VOLUME TREATED, million gallons
        15.9       16.5       18       19.6       21.5
                                             23.1     24.8
                                  I
                               .CLARIFIED EFFLUENT
                            1
                            I
                                'CARBON EFFLUENT
                        •1	1	1	1	1	1	h
                                                              UNIT CONVERSIONS:
                                                              mil gal x 3785= cu m
                                    CLARIFIED EFFLUENT
                                        CARBON EFFLUENT
40       44       48       52
        STUDY PERIOD (WEEKS)
56
60
64
          Figure 31.  Continued

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-pi
              24.8
            10,
         o
         -3 40
         t
         9
         03
         §20
         h-
  TREATED, million gallons
25.6     28.6     30.0
                      68
                                        T
                           T
                                     CLARIFIED EFFLUENT
                                        CARBON EFFLUENT
                                           CONVERSIONS:
                                       mil gal x 3785 =cu m
            CLARIFIED EFFLUENT
                                       CARBON EFFLUENT
                                                 JL
         72       76       80       84
                 STUDY PERIOD (WEEKS)
92
96
         Figure 31. Continued

-------
  30
to  20

Z
ID


-------
en
             30
           05 20
           (T
           o

           O
           O
10
             40
           O
           CD
             20
                        1.8
                        4»
                   i
                   3.4
 5.1
                                VOLUME TREATED, million gallons


                                              CLARIFIED EFFLUENT
                               CARBON EFFLUENT
                                              UNIT CONVERSIONS:
                                              mil gal x 3785= cu m
                                 CLARIFIED  EFFLUENT
                                 CARBON EFFLUENT
                                                   _L
                   8
  12       16       20

STUDY PERIOD (WEEKS)
24
28
32
          Figure 33.Turbidity and  color  removal through the  carbon column- third cycle.

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TABLE 8.   CARBON COLUMN PERFORMANCE
Parameters
Total COD:
Influent,
Effluent,
Removal , %
Dissolved
Influent,
Effluent,
Removal , %
Color:
Influent,
Effluent,
Removal , %
Suspended
Influent,
Effluent,
Removal , %
Turbidity:
Influent,
Effluent,
Removal , %
mg/1
mg/1
COD:
mg/1
mg/1
color units
color units
Solids:
mg/1
mg/1
JTU
JTU
Adsorption
1
98.4
23.6
76.0
48.0
16.1
66.5
19.2
9.8
49.0
30.9
8.3
73.1
24.4
7.7
68.4
2
86.2
10.0
88.4
48.4
7.2
85.1
20.4
6.0
70.6
22.8
4.0
82.5
19.9
3.8
80.9
Cycles
3
98.2
11.5
88.3
52.1
9.4
81.9
21.6
4.7
78.2
24.5
3.8
84.5
20.6
3.6
82.5
Overall
Averages
95.8
19.3
79.9
48.6
13.5
72.2
20.0
7.8
61.0
28.3
6.7
76.3
22.9
6.3
72.5
                 77

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     The apparent density test was  used as  the primary control  test during
regeneration with the decolorizing  tests for iodine and molasses numbers
used as supplemental  control  tests.   The apparent density,  which usually
ranged from 0.48 to 0.49 g/cm3 for  virgin carbon, increased to  about 0.59
to 0.63 g/cm3 when the carbon becomes exhausted.   When the  spent carbon is
properly regenerated, most of the adsorbed  impurities  are removed thus
restoring the apparent density to the virgin level.

     During regeneration, the apparent density test was determined routinely
every hour whereas the tests  for iodine and molasses numbers were performed
every 4 and 2 hours, respectively.   The hourly samples of regenerated and
quenched carbon were composited over the regeneration  period and analyzed
along with the spent carbon composite sample for apparent density, iodine
number, molasses number, methylene  blue number, ash content, and particle
size distribution.

Effect of Regeneration on Carbon Properties

     As a result of thermal regeneration, some losses  inevitably occur both
in the carbon adsorptive capacity and the carbon quantity.   These losses
are of economic importance since they constitute a significant  portion of
the carbon regeneration cost.  The  carbon loss during  the three regeneration
cycles varied from 2.5 to 6 percent.   In this report,  the carbon loss is
defined as the difference in  the carbon volume in the  contactor just before
transfer to the drain bin and just  after backwash of the regenerated carbon.
The carbon loss can be ascribed either to the direct oxidation  of the ex-
terior surfaces of the carbon granules by the activating gases  and/or to
the normal handling attrition if the basic  carbon structure had been prev-
iously weakened by internal over-activation (11).

     The complete removal of adsorbed organics from the carbon  pores is
actually never attained during regeneration.  In addition to ash buildup
in the carbon pores, some of the carbon granules are unavoidably burned
with the adsorbate thereby reducing further the total  surface area available
for adsorption.  Consequently, with the physical  loss  of carbon during
regeneration is the attendant decrease in the adsorptive capacity as
measured by DCOD removal, iodine number and molasses number.

     The changes in some of the physical properties of the  carbon before
and after regeneration are shown in Table 9.  It is apparent from fhe data
that repeated thermal regeneration  had the  effect of decreasing the iodine
number and increasing the ash content.  The iodine number,  which relates
to the surface area of pores  larger than 10 A° diameter, was used in this
study as an index to measure  the extent to  which the carbon micropores were
cleared of adsorbate during regeneration.  As indicated by  the  data in
Table 9, the iodine number decreased about 26 percent from a virgin level
of 1040 to 773 mg/g after three adsorptive  cycles.  The ash content of the
carbon, which measures the amount of calcium and other inorganic residues
picked up by the carbon during service increased about 67 percent from a
virgin level of 6.4 to 10.7 percent after the first regeneration.  On the
                                     78

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TABLE 9.   EFFECT OF REGENERATION ON THE IPC CARBON CHARACTERISTICS
Carbon
Characteristics
Iodine No. , mg/g
Apparent Density,
g/cm3
Molasses No.
Methylene Blue No. ,
mg/g
Ash, %
Mean Particle Dia. ,
mm
Virgin
Carbon
1040
0.484
222
259
6.4
1.44
Spent Carbon
(Composite Sample)
1st
Req.
402
0.629
120
147
10.3
1.46
2nd
Req.
572
0.585
168
153
8.22
1.58
3rd
Req.
570
0.594
154
153
8.67
1.48
Regenerated Carbon (Composite Sample)
Before Quench
1st
Req.
805
0.528
213
223
10.7
1.57
2nd
Req.
722
0.537
233
243
11.6
1.50
nq
3rd
Req.
773
0.526
230
246
7.81
1.54
After Quenching
1st
Req.
751
0.565
189
227
12.0
1.55
2nd
Req.
727
0.548
221
239
12.2
1.50
3rd
Req.
721
0.535
204
245
9.0
1.43

-------
second regeneration, only a slight increase in ash content was observed with
a decrease noted  in the third regeneration.   With the ash buildup following
repeated regenerations, was a corresponding increase in the apparent density
from 0.484 to 0.528 g/cm3.

     In the course of repeated thermal  regenerations some degree of internal
overactivation may occur which eventually results in an increase in macro-
pore volume.   The molasses  number, which relates to surface area of pores
larger than 28 A° diameter, is taken as a measure of pore enlargement.
Another parameter used to measure pore  enlargement during thermal  regener-
ation was the methylene blue number, which relates to surface area of
carbon pores  larger than 15 A° diameter.

     While the iodine number decreased  after repeated regeneration cycles,
both the molasses and methylene blue numbers of the regenerated carbon
remained at about the same  levels as those of the virgin carbon.  This
observation suggests that a portion of  the microspores had not been cleared
of adsorbate  and that a shift of pores  to larger size due to internal
damage of the carbon pore structure, was obviated during the regeneration.

     Table 10 summarizes the furnace operating data for the three  regenera-
tion  cycles.  The data show some variations in the duration of the regen-
eration run,  furnace loading rate and fuel used.  The variations in the
furnace operation have been attributed  to the varying degrees of operating
problems encountered during the regeneration.  The first and third
regenerations preceded without any major operational difficulties.

     During the second regeneration cycle, the regeneration run was stopped
after 36 hours of continuous furnace operation because problems which
developed in  maintaining proper carbon  feed rate to the furnace caused  a
rapid rise in the temperature within the baghouse; eventually resulting in
the burning of all the nomex felt filter bags.  In the second half of the
regeneration, the furnace was operated  only between 6 and 8 hours/day,
instead of the usual continuous furnace operation.  The carbon loss was
estimated at  6  percent, which was much higher than 2.5 percent carbon  loss
observed during the first carbon regeneration.  The high carbon loss could
be attributed primarily to  the intermittent mode of regeneration.   Moreover,
in the second regeneration, difficulties were encountered not only in the
carbon feeding to the furnace but also  in the frequent plugging of the
quench tank screen with gravel.  Apparently, some of the gravel frt5m the
column underdrain system was carried over with the spent carbon during  the
hydraulic transfer to the drain bin.

     Despite  these permanent changes in carbon characteristics as  a result
of regeneration, based on organics removal, the regenerated carbon was  as
good as or better than the  control
                                     80

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                      TABLE 10.   FURNACE OPERATING CONDITIONS DURING IPC CARBON REGENERATION
co
Parameters
Duration of Regeneration, hours
Furnace Loading, Kg carbon/hr (Ib/hr)
Steam Used, Kg/Kg carbon
Fuel Used Kj/Kg Carbon
(BTU/lb Carbon)
Average
Temp. ° C
(° F)

Furnace
Afterburner
Total

Hearth
Number


1
2
3
4
5
6
Afterburner
Carbon Loss, %
Regeneration Number
1 2 3
53 66 60
41.4 (91.1) 34.8 (76.6) 38.3 (84.3)
0.58 0.68 0.62
8427 (3620) 10,086 (4332) 7184 (3086)
7378 (3148) 12,573 (5400) 9764 (4194)
15,756 (6768) 22,660 (9730) 16,948 (7280)
367 (693) 338 (641) 337 (639)
485 (905) 470 (878) 449 (840)
596 (1108) 590 (1095) 558 (1037)
925 (1699) 900 (1652) 896 (1646)
975 (1788) 936 (1717) 942 (1728)
958 (1760) 954 (1750) 946 (1736)
741 (1368) 726 (1339) 719 (1326)
2.5 6 4.4

-------
Air Pollution Control  System Performance

     The flue gases  discharged  from the top  hearth  of  the  multi-hearth  fur-
 nace contained both particulate  and obnoxious-smelling  substances.   These
 air pollutants were controlled through an air  pollution control  system con-
 sisting of a baghouse for particulate  removal  and  an  afterburner,  operated
 in series with the  baghouse for  odor control.   The afterburner was  operated
 at a temperature range of 719°C  (1326°F)  to 741°C  (1368°F).   The baghouse
 was operated at a temperature  ranging  from  149°C  (300°F)  to  163°C  (325°F).
 While it is advantageous  to maintain a high temperature in  the baghouse to
 prevent condensation  problems, due precaution  had  to  be exercised  to prevent
 the temperature from rising to within  10°C  (50°F)  to  38°C (100°C)  of the
 critical temperature  of the fabric filter.   Thus,  to  minimize the  danger of
 burning the filter  bags,  the baghouse  inlet was equipped  with a  valved side
 connection for dilution air addition.  Under normal furnace  operating  condi-
 tions, the dilution air inlet  valve was maintained in a closed position.
 However, when the baghouse temperature increased beyond 163°C (325°F),  which
 could have been triggered by a disruption of the carbon feed rate  and/or
 plugging of the quench tank screen, the dilution air  valve was manually
 opened for such a duration as  needed to restore the temperature  to  about
 163°C (325°F).

     During the first  carbon regeneration, the  performance of the various
 components of the air pollution  control system was evaluated by  test
 engineers from a local testing laboratory.   In evaluating the system,  the
 flue gases at the inlet and outlet of  the baghouse and  at the outlet of the
 afterburner were tested for flow rate, temperature, particulate  matter,
 volatile hydrocarbons, oxygen, carbon  dioxide, carbon monoxide,  water  vapor,
 oxides of nitrogen, and oxides of sulfur.   The odor number was determined on
 the integrated flue gas samples  collected in 8.2-liter  cylinders at the
 inlet to the baghouse and at the outlet of  the afterburner.

     Gas flow measurements were made with  a  standard pi tot tube and  a
 magnehelic draft gauge.  Temperatures  were  measured with  a  Chromel-Alumel
 thermocouple and a  portable potentiometer.   The test  for  particulate matter
 was performed using a wet impingement  method.   Samples  for  the determination
 of oxides of sulfur were  collected by  an  impinger  train containing  hydrogen
 peroxide.  An Orsat analysis was performed  to  determine the  carbon  dioxide
 and oxygen concentrations.  The  phenol-disulfonic  acid  method was  employed
 for the determination of the oxides of nitrogen.   A gas-chromatogwaph-comb-
 ustion-infrared technique was  used to  determine the concentration  of carbon
 monoxide and volatile hydrocarbons.

     During regeneration,  odors were detected and this was confirmed by the
 relatively high odor number of 3 odor  units/1  (90  odor  units/SCF).   Particu-
 late emission was also high and  averaged  0.30  kg/hr (0.64 Ib/hr).   Based on
 the particulate emission  rate  data, the baghouse  removed  only about 26
 percent of the incoming dust load, which  was indeed significantly  below the
                                     82

-------
design removal efficiency of 99 percent.  It should be pointed out, however,
that the emission data represented samples collected over 45 to 60 minutes
sampling period.  The total actual weight of dust collected from the bag-
house over the 53-hour regeneration period was only 14.7 Kg (32.5 Ibs.),
which represented about 56 percent of the calculated dust removed.

    In Table 11 is presented a summary of the emission data from the various
components of the air pollution control system.  For purposes of comparison,
the emission data obtained during the third regeneration of the lead con-
tactor of the tertiary two-stage carbon adsorption system is also included
in this table.  It is apparent from the data in Table 11 that the emission
parameters evaluated were significantly higher in the IPC carbon regeneration
than in the carbon column III 3A.  This observation was expected, considering
that the IPC carbon column was subjected to a much heavier load of organic
matter than column III 3A.  At the time the IPC column was taken off-stream
for regeneration, it had processed 113,550 m3 (30 million gallons) of alum-
polymer treated raw sewage with an equivalent total organic loading of 4.6
kg TCOD applied/kg carbon and 2.3 kg DCOD applied/kg carbon.  The correspond-
ing carbon capacity in the virgin cycle was 3.54 kg TCOD removed/kg carbon
and 1.54 kg DCOD removed/kg carbon.  On the other hand, when column III 3A
was regenerated it had treated 108,000 m3(28.48 million gallons) of activated
sludge plant effluent with a total applied organic loading of 1.0 kg TCOD/
kg carbon and 0.65 kg DCOD/kg carbon.  The COD removal capacity was .65 kg
TCOD/kg carbon and .29 kg DCOD/kg carbon.  The results of the air pollution
control system evaluation thus demonstrate that, the air pollutants eventual-
ly discharged to the atmosphere during carbon regeneration, depend on the
amount and composition of the adsorbate.

DISCUSSION OF THE IPC SYSTEM PERFORMANCE
    As discussed in previous sections the chemical clarification step provided
the major bulk of the pollutant's removal in the IPC system.  In addition to
the anticipated high degree of suspended solids and phosphate removal, sig-
nificant removal of suspended organic material was obtained.  The dissolved
organic removal, however, which was measured by DCOD was only marginal, indi-
cating that the alum-polymer treatment was not effective in the coagulation
of impurities in the wastewater filterable through a 0.45y filter used in the
DCOD determination.  This observation is contrary to what other investigators
(3,12) reported, which suggests that the type of wastewater treated affects
the degree of soluble organics removal  by the chemical clarification process.

    The chemical clarification of raw sewage using alum at an average dosage
of 25 mg/1 Al (275 mg/1  alum) with 0.3 mg/1 of anionic polymer (Calgon WT-
3000) was very effective throughout the study in producing good quality
clarified effluent.  The clarified effluent had an average turbidity, suspend-
ed solids and TCOD concentration of 22.9 JTU, 28.3 mg/1 and 95.8 mg/1, respec-
tively.  The total phosphate in the raw sewage, which had averaged 11.1 mg/1
P was reduced about 88 percent, resulting in a clarified effluent with an
average total phosphate concentration of 1.3 mg/1 P.

    The economics of any chemical clarification system is influenced
a great deal by the cost involved in the treatment'and subsequent disposal
                                      83

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                         TABLE  11.   SUMMARY  OF AIR POLLUTION  CONTROL  SYSTEM PERFORMANCE
Parameters
Parti cul ate Matter
Concentration, mg/1
Emission Rate, kg/hr
. Oxides of Nitrogen ,(NOV)
A
Concentration, mg/1 dry
Emission Rate, kg/hr
. Oxides of Sulfur (S02)
Concentration, mg/1 S02
Emission Rate, kg/hr
. Hydrocarbons
Concentration, mg/1 C
Emission Rate, kg/hr
. Carbon Monoxide (CO)
Concentration, % vol. dry
. Odor
Odor Units/1
*
Gas Flow
Temp. ,° C
Rate, I/sec
APCD
Emission
Limit
0.46
0.45
225.00
2000.00
1st Regeneration of
IPC Carbon Column
Baghouse
Inlet Outlet
7.82 3.57
2.11 1 . 44
49.00 120.00
0.016 0.068
Nil
Nil
5530.00 2800.00
0.74 0.56
5.00 1.7
777.00
271.00 121.00
75.00 112.00
Afterburner
Outlet
0.48
0.30
423.00
0.49
729.00
1.17
221.00
0.066
0.47
3.00
665.60
167.00
3rd Regeneration of Two-
Stage Carbon Column (III 3A)
Baghouse
Inlet Outlet
4.16 1.08
0.98 0.36
40.00
0.012
Nil Nil
740.00 561.00
0.09 0.095
1.36 0.86
706.00
177.80 70.60
66.00 93.00
Afterburner
Outlet
0.017
0.11
180.00
0.18
149.00
0.26
Nil
0.11
0.70
620
177.4
co

-------
of the chemical-sewage sludge produced.  In this study, the flow of the
alum-sewage sludge produced, which was about 1.2 percent of the pilot
plant flow, was of the same level as that normally obtained for waste
activated sludge.  Results of bench-scale studies performed in the course
of the study showed that the alum-sewage sludge was difficult to dewater
and that chemical conditioning at a cost of $15-$17 per ton dry solids was
required to achieve a yield of 4.9-9.8 kg/m -hr (1-2 Ib/ft -hr) with cake
solids of 18 percent.  The economic analysis, which is discussed in subse-
quent sections, showed that the sludge treatment accounts for about 59 per-
cent of the capital cost of the chemical clarification system.

     The function of the subsequent carbon adsorption step is the removal of
residual dissolved organics from the chemical clarification system.  Since
inert media filtration was not provided, the carbon contactor also served as
a deep bed filter for the removal of suspended solids from the clarified
effluent feed.  Because of the suspended solids load as well  as the biologi-
cal growths produced within the column, daily backwashing was required to
relieve the column of excessive headless and to minimize septicity in the
column.  Despite the daily backwashing, sulfide generation still occurred
in the column.  Of the various sulfide control methods evaluated, continuous
sodium nitrate addition to the column at a dosage of about 5.4 mg/1 N was
found to be the most effective.  Moreover, the sodium nitrate added to the
column enhanced the biological activity within the column resulting in
improved overall dissolved organics removal.  In comparing the organic
removal before and after sodium nitrate addition, it was demonstrated that,
indeed, nitrate addition brought about a significant increase in the
capacity of the carbon for DCOD removal.  While the carbon DCOD removal
capacity tends to decrease with repeated thermal regeneration as had been
shown from previous study at Pomona (7), results from the current study has
demonstrated higher carbon capacity of the regenerated carbon compared to
that of virgin carbon.  This result may be due to enhanced biological
activity within the column brought about by the nitrate addition, rather
than a change in the carbon adsorptive property.

     A summary of the overall performance of the IPC pilot plant is present-
ed in Table 12.  The values shown in the table are the average effluent
quality characteristics and removal efficiencies obtained during the entire
27 months of the study.  For purposes of comparison, the effluent quality
from a 30,280 cu m/day (8 mgd) activated sludge plant treating the same raw
sewage is also included in Table 12.  The data clearly demonstrate the
superiority of the IPC system effluent quality over that of the secondary
effluents.

Effect of Copper Waste on IPC System

     One of the main advantages of the physical-chemical treatment system
over biological secondary treatment processes is the ability of the IPC
system to consistently produce good quality effluent even in the presence
of toxic industrial wastes.  The stability of the IPC system operation was
                                     85

-------
                TABLE  12.    SUMMARY OF  IPC SYSTEM PERFORMANCE'
Parameters
Suspended Solids, mg/1
Turbidity, JTU
TCOD, mg/1
gDCOD, mg/1
BOD5, mg/1
Total Phosphate, mg/1 P
Nitrate, mg/1 N
Color
PH
Raw
Sewage
199

321
49.4

11.1


7.7
Clarified
Effluent
28.3
22.9
95.8
48.6
36.2
1.3
0.90
20.0
6.8
Carbon
Effluent
6.7
6.3
19.3
13.5
7.8
0.90
1.3
7.8
6.8
Average
Chemical
Treatment
85.8

70.2
1.6

88.3



Percent Removal
Carbon
Treatment Overall
76.3 96.6
72.5
79.9 94.0
72.2 72.7
78.5
30.8 91.9

61.0

Activated
Sludge
Plant
Effluent
11.6
7.7
39.5
25.7
8.0


33.1

*  Average alum dosage = 25 mg/1 Al (275 mg/1 alum);  Average polymer dosage = 0.3 mg/1  Calgon WT-3000-

-------
indeed demonstrated during a one-week period when the Pomona activated
sludge plant suffered a severe upset caused by a discharge of copper-
bearing wastes.  The measured copper concentration in the sewage for the
24-hour period from March 13 to March 14, 1972 was 1.2 mg/1  Cu.   As
expected, the activated sludge plant effluent quality deteriorated, as
shown by the high levels of suspended solids and COD, whereas, the IPC
effluent quality remained essentially unchanged.  Figures 34 through 36
clearly demonstrate the superiority of theIPC  system  performance over
that of the activated sludge process especially during periods when copper
wastes were present in the incoming raw sewage.

Metals and Miscellaneous Analyses

    Periodically during the course of the study, determination of heavy
metals and other chemical  analyses were performed on the various waste
streams on the IPC system.  The results of the metal analyses are present-
ed in Table 13.  The data indicate that the metal constitutents  in the
carbon effluent were generally low except for iron and zinc which were
significantly higher than those present in the chemically clarified effl-
uent.  The agressive environment within the carbon column produced by ana-
erobic conditions, and the presence of organic sulfides and sulfate-reducing
bacteria could have contributed to the process of corrosion.  Although the
interior of the column was initially coated with coal tar epoxy  to inhibit
corrosion, there could have been some areas which were not properly coated.
In fact, when the column was taken off stream for repairs as discussed
previously, (Dec. 1972 - Jan. 1973), there were some parts where the coat-
ing separated from the column exposing the metal.  This exposed  metal  was
covered with heavy brush-on coat of bitumastic coal  tar epoxy before the
column operation was resumed.  In subsequent periods, the concentrations
of zinc and iron were still high indicating active corrosion taking place
within the column.  The extent of corrosion within the column became
evident in the last two months of the study when leaks occurred  at several
places along the carbon column.

    Table 14 presents the results of mineral analyses and other determina-
tions.  As indicated in the table, the alkalinity, sulfate,  total dissolved
solids and conductivity of the wastewater showed significant changes in
passing through the various stages of the IPC system.  As a result of the
alum addition, sulfate was added to the wastewater in an amount  equivalent
to 5.2 mg/1 SOLf per mg/1  Al added compared to the theoretical value of 5.4
Other soluble wastewater components, however, such as phosphate  and alka-
linity were reduced in concentration, the net effect of which was a slight
increase in the clarified effluent total dissolved solids (TDS)  concen-
tration.  A slight increase in the TDS concentration occurred in the carbon
effluent as a result of sodium nitrate addition to the column for sulfide
control.  As indicated in the table, the conductivity of the effluents also
increased correspondingly.

    Although a high alum dosage ranging from 22-25 mg/1 Al  (242-275 mg/1
                                     87

-------
              120
co
co
              100
              80
           e
           ~  eo
          Q
          O
          o
              40
              20
                                                             ACTIVATED SLUDGE EFFLUENT
                                                                       TCOD
                                                IPC EFFLUENT TCOD
                     ACTIVATED SLUDGE EFFLUENT
                               DCOD
                                          J_
         IPC EFFLUENT DCOD
         __1	I
               I
                                  10
  15        20
MARCH 72	
25
                                                DATE
 30    5        10
-H-*	—APRIL'
15
          Figure 34. Effect of  copper  waste on the COD  removal.

-------
CO
to
                                                       •ACTIVATED SLUDGE EFFLUENT
                                                        b-cf
                                                  IPC EFFLUENT
                                                  DATE
         Figure 35. Effect of copper waste on  suspended solids  removal.

-------
    60
    50
    40
   ' 30
  Q
  GO
    20
     10
                                            ACTIVATED SLUDGE EFFLUENT
 10        15       20
	MARCH 72	
                                                   25
30    5        10
3^U      APRIL-
                                        DATE
Figure 36. Effect of  copper waste  on  turbidity  removal.

-------
TABLE 13.   HEAVY METAL ANALYSES
Constituents
(ug/D
Aluminum
Arsenic
Boron
Cadmi urn
Chromium (Hex. )
Chromium (Total )
Copper
Cyanide
Fluoride
Iron
Lead
Manganese
Mercury
Nickel
Silver
Zinc
Raw
Sewage
70.0
22.0
720.0
4.0
45.0
238.0
830.00
25.0
890.0
880.0
185.0
16.0
0.8
190.0
4.2
217.0
Clarified
Effluent
336.0
9.1
429.0
2.9
36.0
110.0
275.0
19.1
303.0
228.0
366.0
17.5
0.3
182.0
1.8
257.0
Carbon
Effluent
50.0
7.0
610.0
2.6
2.3
25.0
71.0
11.5
290.0
928.0
28.5
20.0
0
105.0
6.7
587.0
Average Removal , %
Chemical
Treatment
--
58.6
40.4
27.5
20.0
53.8
66.9
23.6
66.0
74.1
80.2
—
66.7
4.2
57-1
--
Carbon
Column
85.1
23.1
--
10.3
93.6
77.3
74.2
39.8
4.3
--
22.1
—
100.0
42.3
--
--
                91

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TABLE 14.    MINERAL AND MISCELLANEOUS ANALYSES
Constituents
Alkalinity, mg/1 CaC03
Calcium, mg/1 Ca
Chloride, mg/1 Cl
Magnesium, mg/1 Mg
Nitrate, mg/1 N
Potassium, mg/1 K
Sodium, mg/1 Na
Sulfate, mg/1 SO^
MBAS, mg/1
Phenols, mg/1 phenol
2
Conductivity, umhos/cm
Total dissolved solids, mg/1
PH
Raw Sewage
217.00
51.30
104.40
10.90

10.50
100.00
95.00
1.96
0.17

573.00
7.68
Clarified
Effluent
130.00
52.8
105.40
11.20
0.90
10.80
101.00
225.00
2.42
0.055
1046.00
618.00
6.75
Carbon
Effluent
169.00
52.4
96.20
11.00
1.32
11.40
113.00
219.00
0.43
0.005
1089.00
627.00
6.80
                     92

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alum) was used in the chemical clarification of the raw sewage, the clar-
ified effluent and carbon effluent contained only 0.31  and 0.05 mg/1  Al,
respectively.  The alum floe in the clarified effluent was effectively
filtered out in the carbon column.  While most of the trapped floe was
removed from the carbon column during the routine backwash operation,
invariably some floe adhered tenaciously to the carbon granules.

     In an effort to determine the fate of various metals present in  the
chemically clarified effluent in passing through the carbon column,
samples of virgin carbon, spent carbon and quench water were collected
during the first carbon regeneration.  These samples were analyzed for
various metal constituents at the Municipal Environment Research Lab-
oratory of the U.S. EPA in Cincinnati, Ohio.  The summary of the test
results are presented in Table 15.  In evaluating the data from this  table,
the following general observations can be drawn:

(1)  The spent carbon contained considerably larger concentrations of Cd,
     Cr, Cu, Ni and Zn than were present in the virgin carbon.   Analyses
     of spent carbon taken at various depths of the column showed the
     amount of Cd, Cr, Cu and Zn were highest at the top  30.5 cm
     (12 in.) of the carbon bed with the concentration of nickel  about
     evenly distributed throughout the bed.  The concentrations of Hg,
     Ti, Be, As and Sr in the spent carbon were lower than that in the
     virgin carbon.

(2)  The concentrations of Zn3 Cr, Cu and Ni in the regenerated carbon
     were much higher than those of virgin carbon.  In comparing the
     metal contents of the spent carbon composite samples with  those
     of the 12-hr.regenerated carbon composite samples, it is apparent
     that a high loss of Cd and small losses of Zn, Crs Cu, As, Fe
     and Pb occurred on regeneration.

(3)  The baghouse dust contained considerably higher levels of Ca, Cd,
     Cu, Cr, Al, Fe, Sr, Sn, Pb, Ni,and Zn  than virgin carbon.

(4)  The metal constitutents in the quench water were found generally
     near background levels.

(5)  Unlike the other metals, Cd was almost completely stripped from
     the carbon during regeneration and ended up in the baghouse.

     The changes in the various forms of nitrogen during chemical treat-
ment and subsequent carbon adsorption are presented in Table 16.   The
ammonia concentration increased from 14.5 mg/1 N in the raw sewage to
21.2 mg/1 N after chemical clarification and remained essentially un-
changed in passing through the carbon column.  However, the organic
nitrogen  concentration showed a significant drop from 14.7 in  the raw
sewage to 6.3 mg/1 N in the clarified effluent and to a level  of 2.1
mg/1 N after  carbon adsorption.  The nitrate concentration in  the
                                    93

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      TABLE 15.   HEAVY METAL CONSTITUENTS OF QUENCH WATER AND CARBON SAMPLES
Metal
Hg
Se
Sb
Sn
Co
Tl
Mo
Ti
V
Be
Bi
Zn
Cr
Pb
Ni
Mn
Cu
Ba
Cd
As
Fe
Al
Sr
Ca
Virgin
Filtrasorb
300
1.92
<0.96
<7.20
<48.00
<4.80
<24.00
<12.00
240.00
24.00
2.40
<24.00
1.20
7.20
16.80
12.00
26.40
<1.20
50.40
1.20
108.00
617.00
1536.00
72.00
391.00
Spent Carbon
Composite
0.36
<.96
<7.20
72.00
14.40
<24.00
<12.00
96.00
24.00
<2.40
<24.00
132.00
658.00
19.20
816.00
1.20
444.00
76.80
26.40
57.60
1200.00
1920.00
|8. 40
3120.00
Avg. of 4-12 hr Composites
of Regenerated Carbon
0.45
9.84
<7.20
<48.00
24.00
<24.00
<12.00
216.00
24.00
<2.40
<24.00
102.00
559.80
13.80
936.00
30.60
286.30
79.20
<1.20
49.80
912.00
3162.00
80.40
4632.00
Avg. of 4-12 hr Composites
of Quench Water *

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                    TABLE 16.   NITROGEN REMOVAL IN THE IPC SYSTEM
Nitrogen
Forms
(mg/1)
Organic N
NH -N
3
NO -N
2
NO -N
3
Total N
Raw
Sewage
14.7
14.5
0.8
2.6
32.6
Clarified
Effluent
6.3
21.2
0.4
0.9
28.8
Carbon
Effluent
2.1
21.3
0.2
(*)
1.31 '
24.9

Chemical
Treatment
57.1
__
50.0
65.4
11.7
Percent Removal
Carbon
Treatment
66.7
—
50.0
79.4 ^+>
27.2

Overall
85.7
—
75.0
1
1
*  Sodium nitrate fed to carbon column = 4.5 - 5.8 mg/1 N
+  Based on an average sodium nitrate fed to column =5.4 mg/1

-------
carbon effluent averaged 1.3 mg/1  N which was  slightly higher than that of
the clarified effluent.   The nitrate, which was added to the carbon column
at dosages from 4.5 - 5.8 mg/1  N for sulfide control  was completely reduced
presumably by biological denitrification in the carbon column.   The
significant increase of the ammonia level in the clarified effluent was
probably due to the biological  oxidation of the organic nitrogen in the
raw sewage and/or in the alum-sewage sludge.
                                    96

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                            SECTION 6

                        ECONOMIC ANALYSIS


     For convenience in the discussion of the economic analysis, the
estimated treatment cost for the IPC system is subdivided into three parts,
namely,  chemical treatment costs, carbon treatment costs and total  IPC
system costs.  The economic analysis is based on the treatment of Pomona
wastewater for an average design flow of 0.44 m3/sec (10 mgd) and a  peak
design flow of 0.61 m3/sec (14 mgd).  The process design parameters  for
sizing the various treatment units are presented in Table 17.  The assumed
unit costs for chemicals and other direct costs for estimating the operation
and maintenance (0/M) costs are shown in Table 18.  Figure 37 presents the
IPC system flowsheet, showing the various treatment components employed.

     In the preparation of the economic analysis, various published  reports
were consulted, particularly references (13,14) for the chemical treatment
system and reference ( 6) for the carbon contacting system.   The capital
costs obtained from literature were adjusted to reflect the  price levels
of March 1975, with an EPA sewage treatment plant construction cost  index
of 232.1.

CHEMICAL TREATMENT COSTS

     Table 19 presents a summary of the chemical treatment costs for a  0.44
m3/sec (10 mgd) plant.  The estimated capital  costs of the various treatment
components include allowance for instrumentation, pipings, appurtenances
and buildings.  In addition, an allowance of 20 percent of the total  capital
costs is included for engineering, legal  and administrative  costs.  The
preliminary treatment costs include the costs  for bar screening, comminution,
grit removal  and flow measurement.

     The costs in Table 19 sJnow that about 59  percent of the total capital
costs is associated with the treatment and disposal of the alum-sewage
sludge produced in the chemical coagulation-sedimentation system.  Of the
total chemical treatment cost of 5.29 i/m3 (19.81 <£/1000 gallons), 67
percent represents operation and maintenance (0/M) and only  33 percent for
capital amortization.   Moreover, about 67 percent of the 0/M costs is
associated with the cost of alum and polymer used in the chemical
clarification of the raw sewage.
                                     97

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             TABLE 17.    IPC SYSTEM DESIGN  DATA
CHEMICAL TREATMENT SYSTEM

     1.   F1peculation:
          Detention Time, minutes                        45.0
          Chemical Dosage
                    Alum, mg/1   Al                       22.0
                    Polymer,  mg/1                         0.25

     2.   Sedimentation:
          Detention Time, hours                           1.5
          Overflow Rate,  cu m/day/m2                    36.6
          Underflow, %  of plant  flow                     1.25
          Underflow solids, % by weight                  2.0

     3.   Gravity Thickening:
          Solids Loading, kg/day-m2                     58.0
          Underflow solids, % by weight                  4.0

     4.   Vacuum Filtration:
          Yield,kg/hr-mz                               9.8
          Cake solids                                   18.0

     5.   Sludge Incineration:
          Solids Loading, Kg/hr-m2                       9.8
CARBON TREATMENT SYSTEM

     1.  Carbon Contacting (8 x 30 mesh carbon)
          Empty-bed contact time                        25.0
          Hydraulic surface loading,  1/sec/m2            2.7
          Backwash volume , % of plant flow              5.0
          Sodium Nitrate Dosage, mg/1   N                 5.5
          Carbon Dosage,   kg/m3                         0.03
          Carbon Regeneration loss, %                     5.0
                             98

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TABLE 18.   UNIT COSTS FOR OPERATION AND MAINTENANCE ESTIMATE
 CHEMICALS
        Alum, $/kg  Al                                           1.00
        Polymer, $/kg                                            4.40
        Sludge conditioning polymer, $/Ton dry solids           15.00
        Sodium nitrate, $/kg sodium nitrate                      0.16
        Granular activated carbon (8 x 30 mesh), $/kg            1.10
 OPERATING COSTS
        Power, tf/KWH                                             2.0
        Fuel, <£/therm                                           10.0
        Carbon regeneration fuel, Kj/kg                     14,000.00
        Sludge Incineration, $/ton dry solids                    5.0
        Backwash water,  <£/m                                     0.8
        Operating Labor, 5 at $12,000/yr.                    60,000.00
        Maintenance Labor, 2 at $10,000/yr.                  20,000.00
        Laboratory personnel, 1 at $14,000/yr.               14,000.00
        Maintenance materials, $/yr
                  Chemical Treatment                        20,000.00
                  Carbon Treatment                          10,000.00
 CAPITAL COSTS
       All  equipment costs were amortized at 6% for 25  years.
                                 99

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                                    RAW SEWAGE
o
o
                                         I
BA(
| 	
s
s
1
1 so
	 !

PRELIMINARY TREATMENT
:iKWASH_RECYCLE 	
I
I
ALUM 	 >•
POLYMER 	 ^CHEMICAL TREATMENT
[>IUM NITF
1 SPENT
CARBO
CARBON
REGENERATION

PATF -. - ..
f
"~~ GRANULAR
fARRON "

N ^
REGENERATED \\
CARBON jl
t ,
VIRGIN |
MAKE-UP— -1 '
tARBON TRE>
EFFL
L
ACTIVATED
FREATMENT
i
^TED
UENT
THICKENER
ALUM-SEWAGE 	 ^
	 1
1
L_F]LT RATJE __

GRAVITY
THICKENING
(

-*- POLYMER
VACUUM
FILTRATION
\

INCINERATION

I
DISPOSAL
       Figure 37. Proposed IPC system-flow sheet.

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               TABLE 19.    ESTIMATED CHEMICAL TREATMENT COST*
CAPITAL COSTS (1000 of $)

     Raw Sewage pumping station                             388
     Preliminary Treatment                                   85
     Coagulation-Sedimentation                              568
     Gravity Thickening                                      94
     Vacuum Filtration                                      584
     Incineration                                           812
              Total                                       2,531

     Engineering, legal and administrative costs,  (20%)      506
     Total capital costs                                  3,037


     Amortized cost, tf/m3 U/1000 gallons)                      1.74   (6.50)


OPERATION AND MAINTENANCE COSTS  l/m3 U/1000 gallons)

     Treatment Chemicals (alum and polymer)                     2.32   (8.86)
     Sludge Conditioning Chemical (polymer)                     0.42   (1.56)
     Power and Fuel                                             0.28   (1.06)
     Operating and maintenance labor                            0.34   (1.28)
     Maintenance material                                       0-15   _(0.55)_

     Total operating and maintenance cost,
     
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CARBON TREATMENT COSTS

     The carbon contacting system consists of 10 carbon columns operated
in parallel at a design flow of  0.44 m3/sec (1  mgd) per column.  Two
carbon storage tanks, each of which has a capacity equal to that of a
carbon column, is also provided.  One of these storage tanks is initially
charged with carbon while the other tank is reserved for spent carbon
storage.  Thus, the initial  carbon charge is equivalent to the effective
volume of 11 carbon contactors.

     A summary of the estimated carbon treatment costs is presented in Table
20,  As indicated in the cost breakdown, the amortized cost represents
about 2.04 <£/m3 (7.62 it/1000 gallons).  The costs of sulfide control in the
carbon column accounts for 37.5 percent of the total 0/M costs.  The
operating and maintenance labor costs of 0.34 i/m3 (1.28 <£/1000 gallons), is
assumed to be one-half of that of the complete IPC system.

IPC SYSTEM COST

     In Table 21 is shown the complete cost breakdown of the IPC system.
The total treatment cost to  produce carbon treated effluent with character-
istics similar to that presented in Table 8 from 0.44 m3/sec (10 mgd) of
raw sewage is estimated at 8.69 <£/m3 (32.57 <£/1000 gallons).  The effluent
quality from the IPC system  would be about equal  to or slightly better than
that obtained from a secondary biological treatment system for all  the
parameters evaluated.  Moreover, the IPC system  has the added advantage
of not only providing stable effluent quality but also effluent with total
phosphate concentration of 0.9 to 1 mg/1 P.

     The cost data in Table  21 show that the chemical treatment system cost,
which includes the cost for  the treatment and disposal of the alum-sewage
sludge, represents about 61  percent of the total  IPC system process costs.
If regeneration facilities were not required, the total treatment cost
is reduced to 7.92 i/m3 (29.68 <£/1000 gallons).   This 9 percent cost
reduction is important especially in small plants where the regeneration
cost represents a significant portion of the overall cost.
                                    102

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        TABLE 20.   ESTIMATED GRANULAR ACTIVATED CARBON TREATMENT COSTS*
CAPITAL COSTS (1000 of $)

     Influent Pumping                                       219
     Initial Carbon Charge                                  331
     Carbon Contacting System                             1,766
     Carbon Regeneration System                             650
              Total                                       2,966

     Engineering, legal and administrative costs (20%)       593
     Total capital cost                                   3,559

     Amortized cost, tf/m3 U/1000 gallons)                     2.04   (7.62)


OPERATING AND MAINTENANCE COSTS j/m3 (6/1000 gallons)

     Carbon make-up                                            0.16   (  -62)
     Backwash water                                            0.04   (  .15)
     Power and Fuel                                            0.24   (  .89)
     Sulfide control (sodium nitrate)                          0.51   (1.93)
     Operating and maintenance labor                           0.34   (1.28)
     Maintenance material                                      0,-QZ  (  -27)_

     Total operating and maintenance cost,
     <£/m3 U/1000 gallons)                                     1-36  (  5.14)

     Total treatment cost, <£/m3 U/1000 gallons)               3.40  (12.76)


*  Based on EPA sewage treatment plant construction cost index
   of 232.1 (March 1975) for a 37,850 cu m/day (10 mgd)  plant.
                                    103

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               TABLE 21.   ESTIMATED IPC SYSTEM COSTS*
CAPITAL COSTS (1000 of $)

     Chemical Treatment System                         3,037
     Carbon Treatment System                           3,559
     Total Capital Cost                                6,596

     Amortized Cost, 
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                                REFERENCES

 1.   Rizzo, J.L.  and Schade,  R.E.,  "Secondary  Treatment with Granular
     Activated Carbon",  Water and Sewage  Works,  Vol.  116, No. 8, p 307
     (Aug.  1969).

 2.   Hopkins, C.B., Weber,  W.J.,  Jr.,  and Bloom,  R.,  Jr., "Granular Carbon
     Treatment of Raw Sewage", Water Pollution Control Research Series
     ORD 17050 DAL 05/70,  U.S. Department of  Interior, Federal Water
     Quality Administration (May  1970).

 3.   Friedman, L.D., Weber, W.J., Jr., Bloom,  R.,   Jr., and Hopkins, C.B.,
     "Improving Granular Carbon Treatment", Water  Pollution Control
     Research Series  17020 GDN 07/71, U.S. Environmental Protection
     Agency, (July 1971).

 4.  "Standard Methods for the Examination of Water and Wastewater", 13th
     Ed., American Public Health  Association,  New  York, (1971).

 5.   "FWPCA Methods for  Chemical  Analysis of Water and Wastes", Federal
     Water Quality Administration,  Cincinnati, Ohio  (Nov. 1969).

 6.   "Process Design Manual for Carbon Adsorption",  U.S. Environmental
     Protection Agency,  (October  1973).

 7.   Parkhurst, J.D., Dryden, F.D.,  McDermott, G.N.,  and English, J.N.,
     "Pomona Activated Carbon Pilot Plant", Journal  Water Pollution
     Control Federation, Vol. 39, No.  10, part 2,  1270 (October  1967).

 8.   Heukelekian, H. , "Some Bacteriological Aspects  of Hydrogen Sulfide
     Production from Sewage", Sewage Works  Journal,  Vol. 20, No. 3,
     pp 490  (May 1948).

 9.   Dague, R.R., "Fundamentals of Odor Control",  Journal Water Pollution
     Control Federation, Vol. 44, No.  4,  pp 583  (April 1972).

10.   English, J.N., Carry,  C.W.,  Masse, A.N.,  Pitkin, J.B., and Dryden, F.D.,
     "Denitrification in Granular Carbon  and  Sand  Columns", Journal Water
     Pollution Control Federation,  Vol.  46, No.  1, pp 28  (Jan. 1974).
                                     105

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11.   Juhola, A.J.  and Tepper,  F.,  "Regeneration  of  Spent  Granular
     Activated Carbon",  Report No.  TRWC-7,  Robert A.  Taft Water Research
     Center, U.S.  Dept.  of Interior,  Cincinnati, Ohio  (Feb.  1969).

12.   Burns, D.E.  and Shell,  G.L.,  "Physical-Chemical  Treatment  of
     Municipal Wastewater using Powdered  Carbon", Environmental  Protection
     Agency Technology Series, EPA,  R2-73-264, U.S.  Environmental
     Protection Agency (August  1973).

13.   Smith, R., "Electrical  Power  Consumption for Municipal Wastewater
     Treatment",  Environmental  Protection Agency Technology   Series,
     EPA-R2-73-281,  U.S.  Environmental  Protection Agency   (July 1973).

14.   Patterson, W.L., and Banker,  R.F.,  "Estimating Cost  and  Manpower
     Requirements  for Conventional  Wastewater Treatment Facilities",
     Water Pollution Control  Research Series, 17090 DAN 10/71,
     U.S.  Environmental  Protection  Agency   (October  1971).

15.   Lawrence, A.W,  and  McCarty, P.L. ,  "Unified  Basis for Biological
     Treatment Design and Operation", Journal Sanitary Engineering
     Division, Proceedings American  Society  of Civil  Engineering,
     Vol.  96,  SA 3, 757  (1970).
                                   106

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                                   TECHNICAL REPORT DATA
                            (Please read Instructions on the reverse before completing)
1. REPORT NO.
   EPA-600/2-77-137
                                                           3. RECIPIENT'S ACCESSI ON" NO.
4. TITLE AND SUBTITLE
  INDEPENDENT PHYSICAL-CHEMICAL  TREATMENT OF RAW
  SEWAGE
                                              5. REPORT DATE
                                               August  1977  (Issuing Date)
                                                           6. PERFORMING ORGANIZATION CODE
7. AUTHOR(S)
    Leon  S.  Directo, Ching-Lin Chen,  and  Robert P.  Miele
                                              8. PERFORMING ORGANIZATION REPORT NO
9. PERFORMING ORGANIZATION NAME AND ADDRESS

  Los  Angeles County Sanitation  Districts
  Whittier, California 90607
                                              10. PROGRAM ELEMENT NO.
                                                 1BC611
                                              11. CONTRACT/GRANT NO.
                                                             14-12-150
 12. SPONSORING AGENCY NAME AND ADDRESS
  Municipal Environmental Research  Laboratory--Cin.,  OH
  Office  of Research and Development
  Environmental Protection Agency
  Cincinnati,  Ohio 45268
                                              13. TYPE OF RE PORT AND PERIOD COVERED
                                               Final  - Jan.1973-Aug.1975
                                              14. SPONSORING AGENCY CODE
                                               EPA/600/14
 15.SUBP-LEMENTARY JSIOTES
   Project  Officer:   Irwin J. Kugelman  (513-684-7631)
 A'3.T/l/sec(50 gpm)pilot plant  evaluation of the independent physical-chemical  treat-
 ment (IPC)process was condicted  for  27-months at Pomona, California. The  pilot  plant
 consisted of chemical clarification  w/alum at 25 mg/1 as Al and an
 0.3  mg/1  followed by a single-stage, pressurized
 hydraulic loading of 2.71 l/sec/m^(4 gpm/ft2)and
 Performance data obtained have demonstrated the
                                           as Al and an  anionic  polymer at
                                      downflow carbon column  operated at a
                                      an empty-bed contact  time  of 30 min.
                                     stability of the IPC system in produc-
 ing  effluent of excellent overall  quality.   The suspended solids, total COD  and  total
 phosphate removals in the IPC  system were 96.6%, 94%, & 92%, respectively.   In the
 course  of the study, several methods of controlling sulfide generation in the carbon
 column  were evaluated. Continuous  sodium nitrate addition to the carbon column at an
 average dosage of 5.4 mg/1 N was found  most effective in preventing sulfide  generation.
 The  addition of nitrate had another  favorable effect in that it permitted, through
 enhancement of biological activity,  a very high organic loading on the carbon column.
 The  carbon capacity was 3.54 Kg total COD removed/Kg carbon and 1.54 Kg dissolved COD
 removed/Kg carbon. Although regeneration was not necessary, it was conducted in  an
 effort  to obtain data on the effects of repeated regenerations on the carbon character-
 istics.  In all  respects, the regenerations  were as successful as those conducted on
 granular activated carbon used in  the tertiary treatment mode. The performance of the
 regenerated carbon was found equal to or slightly better than that of the virgin carbon
bon
averaged 4.37;  per
Ca
                               DOCUMENT ANALYSIS
                  DESCRIPTORS
                                              b.IDENTIFIERS/OPEN ENDED TERMS
                                                             COS AT I Field/Group
Activated  Carbon
Coagulation
Sedimentation
     Treatment
                                           Nitrate Treatment
                                           Carbon Regeneration
                                           Biological Activity
                                           Sludge Dewatering
                                           Physical-Chemical Treat-
                                            ment
                                                              13B
13. DISTRIBUTION STATEMENT

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EPA Form 2220-1 (9-73)
                                            107
                                                                    
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