EPA-R2-73-149

February 1973
Environmental Protection Technology Series
    Physical -  Chemical Treatment

    of Combined and Municipal Sewage
                         SB
         '4
          111
          CD
                                  Office of Research and Monitoring



                                  U.S. Environmental Protection Agency


                                  Washington, D.C. 20460

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            RESEARCH REPORTING SERIES
Research reports of the  Office  of  Research  and
Monitoring,  Environmental Protection Agency, have
been grouped into five series.  These  five  broad
categories  were established to facilitate further
development  and  application   of   environmental
technology.   Elimination  of traditional grouping
was  consciously  planned  to  foster   technology
transfer   and  a  maximum  interface  in  related
fields.  The five series are:

   1.  Environmental Health Effects Research
   2.  Environmental Protection Technology
   3.  Ecological Research
   4.  Environmental Monitoring
   5.  Socioeconomic Environmental Studies

This report has been assigned to the ENVIRONMENTAL
PROTECTION   TECHNOLOGY   series.    This   series
describes   research   performed  to  develop  and
demonstrate   instrumentation,    equipment    and
methodology  to  repair  or  prevent environmental
degradation from point and  non-point  sources  of
pollution.  This work provides the new or improved
technology  required for the control and treatment
of pollution sources to meet environmental quality
standards.

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                                                EPA-R2-73-149
                                                February 1973
          PHYSICAL - CHEMICAL TREATMENT
                         Of
          COMBINED and MUNICIPAL SEWAGE
                         by

                  Alan J. Shuckrow
                  Gaynor W.  Dawson
                  William F.  Bonner
                 Contract  14-12-519
               Project No.  11020 DSQ
                  Project Officer
               Mr. Danforth G.  Bodien
         Environmental Protection Agency
            Seattle, Washington  98901
                  prepared for the

        Office  of Research  and Monitoring
         ENVIRONMENTAL PROTECTION AGENCY
              Washington, D.C. 20460
For sale by the Superintendent of Documents, U.S. Government Printing Office, Washington, D.G. 20402
               Price $2.35 domestic postpaid or $2 GPO Bookstore

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                      EPA Review Notice

This report has been reviewed by the Environmental Protec-
tion Agency and approved for publication.  Approval does
not signify that the contents necessarily reflect the views
and policies of the Environmental Protection Agency, nor
does mention of trade names or commercial products consti-
tute endorsement or recommendation for use.
                             11

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                          ABSTRACT
A unique physical-chemical wastewater treatment system
utilizing powdered activated carbon was developed and demon-
strated by Battelle-Northwest under contract to the EPA.
The research program included laboratory process development
followed by design, construction, and field demonstration of
a 100,000 gpd mobile pilot plant.

In the treatment process, raw wastewater is contacted with
powdered carbon, coagulated with alum, settled with poly-
electrolyte addition and, in some cases, passed through a
tri-media filter.  The solids from the clarifier, composed
of raw sewage solids, powdered carbon, and aluminum hydrox-
ide floe, are readily dewaterable to 20-25 percent solids
by direct centrifugation with the powdered carbon acting as
a substantial aid to dewatering.  The dewatered solids are
passed through a fluidized bed furnace developed specifi-
cally for powdered carbon regeneration.  Alum is recovered
by acidifying the regenerated carbon slurry from the furnace
to a pH of 2.  The recovered carbon and alum are recycled
as an acidified slurry and added to the raw sewage with the
makeup carbon.

The program demonstrated the ability of the treatment pro-
cess to consistently produce high-quality effluent from raw
wastewater.

Powdered carbon regeneration was highly successful on the
pilot scale.  Full capacity recovery was achieved with less
than two percent carbon loss per regeneration cycle.  Alum
recovery was also greater than ninety percent.

Initial cost estimates, including both operation and capital
amortization, are 16.8^/1000 gal. for combined sewage treat-
ment and 22-23^/1000 gal. for raw municipal wastewater.

This report was submitted in fulfillment of Project # 11020
DSQ and Contract # 14-12-519 under the sponsorship of the
U. S. Environmental Protection Agency.
                            111

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                           CONTENTS






SECTION




  I      CONCLUSIONS




  II     RECOMMENDATIONS




  III    INTRODUCTION




  IV     PILOT  PLANT  DESCRIPTION




  V      DEMONSTRATION SITE




  VI     TREATMENT  SYSTEM PERFORMANCE




  VII    REGENERATION




  VIII   DESIGN AND ECONOMIC CONSIDERATIONS




  IX     ACKNOWLEDGMENTS




  X      REFERENCES




  XI     APPENDIX A
PAGE;



  i



  7



  9



 15



 25



 33



 99



133



141



143



145
                               v

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                            FIGURES


NO.                                                  PAGE

 1     PROCESS  FLOW SHEET                             11

 2     MOBILE PILOT PLANT                             12

 3     SCHEMATIC FLOWSHEET OF MOBILE  PILOT PLANT     16

 4     CHEMICAL INJECTION POINT IN  PIPE REACTOR      17

 5     FLUIDIZED BED REGENERATION UNIT                19

 6     REGENERATION SYSTEM SCHEMATIC  FLOWSHEET       21

 7     PILOT PLANT IN OPERATION AT  ALBANY SITE       22

 8     FLUIDIZED BED CONTROL PANEL                    23

 9     ISLAND CREEK DRAINAGE AREA AND
       DEMONSTRATION SITE LOCATION                    26

10     TYPICAL  DIURNAL DRY WEATHER  FLOW
       VARIATION AT ALBANY SITE                       27

11     AVERAGE  DIURNAL BOD AND COD
       FLUCTUATION AT ALBANY SITE                     29

12     AVERAGE  DIURNAL SUSPENDED SOLIDS AND
       TURBIDITY FLUCTUATION AT ALBANY  SITE          30

13     AVERAGE  DIURNAL PHOSPHATE FLUCTUATIONS
       AT ALBANY SITE                                 31

14     STORM EFFECT ON TURBIDITY
       AND SUSPENDED SOLIDS - 7/13/71                38

15     STORM EFFECT ON COD - 7/13/71                  39

16     STORM EFFECT ON TURBIDITY
       AND SUSPENDED SOLIDS - 7/19/71                40

17     STORM EFFECT ON COD - 7/19/71                  41

18     STORM EFFECT ON TURBIDITY
       AND SUSPENDED SOLIDS - 7/29/71                42

19     STORM EFFECT ON SETTLEABLE SOLIDS  - 7/29/71   43

20     STORM EFFECT ON BOD AND COD  -  7/29/71          44
                               VI

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(FIGURES Continued)
21     STORM  EFFECT ON TURBIDITY AND
       SUSPENDED SOLIDS - 9/13-14/71                  45

22     STORM  EFFECT ON BOD AND COD -  9/13-14/71      46

23     STORM  EFFECT ON TURBIDITY AND
       SUSPENDED SOLIDS - 9/16-17/71                  47

24     STORM  EFFECT ON BOD AND COD -  9/16-17/71      48

25     STORM  EFFECT ON TURBIDITY AND
       SUSPENDED SOLIDS - 5/2/72                      49

26     STORM  EFFECT ON BOD AND COD -  5/2/72           50

27     STORM  EFFECT ON TURBIDITY AND
       SUSPENDED SOLIDS - 5/16/72                     51

28     STORM  EFFECT ON COD AND BOD -  5/16/72          52

29     STORM  EFFECT ON TURBIDITY AND
       SUSPENDED SOLIDS - 5/16/72                     53

30     STORM  EFFECT ON COD AND BOD -  5/16/72          54

31     STORM  EFFECT ON TURBIDITY AND
       SUSPENDED SOLIDS - 5/16-17/72                  55

32     STORM  EFFECT ON COD AND BOD -  5/16-17/72      56

33     JAR TEST DETERMINATION OF CARBON  REQUIRE-
       MENTS  DURING INCREASING AND PEAK  LOADING
       OF  7/29/71 STORM                               58

34     JAR TEST DETERMINATION OF CARBON  REQUIRE-
       DURING DECREASING AND MINIMUM  LOADING  OF
       7/29/71 STORM                                  59

35     PLANT  SUSPENDED SOLIDS AND
       TURBIDITY REMOVAL - 7/12-13/71                64

36     PLANT  COD REMOVAL - 7/12-13/71                65

37     PLANT  SUSPENDED SOLIDS AND
       TURBIDITY REMOVAL - 7/14-15/71                66

38     PLANT  COD REMOVAL - 7/14-15/71                67

39     PLANT  COD AND BOD REMOVAL - 8/17-18/71        68

40     PLANT  COD AND BOD REMOVAL - 9/28-29/71        69
                              vi 1

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 (FIGURES  Continued)


 41     PLANT  SUSPENDED SOLIDS REMOVAL - 10/4-5/71     70

 42     PLANT  COD  AND  BOD REMOVAL - 10/4-5/71          71

 43     PLANT  SUSPENDED SOLIDS REMOVAL - 10/7-8/71     72

 44     PLANT  COD  AND  BOD REMOVAL - 10/7-8/71          73

 45     PLANT  SUSPENDED SOLIDS REMOVAL -
       10/13-14/71                                     74

 46     PLANT  COD  AND  BOD REMOVAL - 10/13-14/71        75

 47     PLANT  COD  AND  BOD REMOVAL - 10/25-26/71        76

 48     PLANT  SUSPENDED SOLIDS AND TURBIDITY
       REMOVAL  -  4/14 & 4/17-19/72                    78

 49     PLANT  COD  AND  BOD REMOVAL - 4/14
       & 4/17-19/72                                    79

 50     PLANT  SUSPENDED SOLIDS AND
       TURBIDITY  REMOVAL -  4/24-26/72                 80

 51     PLANT  COD  AND  BOD REMOVAL - 4/24-26/72         81

 52     PLANT  SUSPENDED SOLIDS AND TURBIDITY
       REMOVAL  -  5/1-3/72 &  5/9-10/72                 82

 53     PLANT  COD  AND  BOD REMOVAL -
       5/1-3/72 & 5/9-10/72                            83

 54     PLANT  TURBIDITY AND  SUSPENDED SOLIDS
       REMOVAL  -  5/16-17/72  & 5/23/72                 84

 55     PLANT  COD  AND  BOD REMOVAL -
       5/16-17/72 & 5/23/72                            85

 56     PLANT  TURBIDITY AND  SUSPENDED SOLIDS
       REMOVAL  -  6/7-8/72 &  6/12/72                   86

 57     PLANT  COD  AND  BOD REMOVAL -
       6/7-8/72 & 6/12/72                             87

 58     PLANT  TURBIDITY AND  SUSPENDED SOLIDS
       REMOVAL  -  6/13-15/72                            88

 59     PLANT  COD  AND  BOD REMOVAL - 6/13-15/72         89

60     FREQUENCY  DISTRIBUTION OF PILOT
       PLANT  EFFLUENT  QUALITY                         90
                              VI11

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(FIGURES Continued)
61     CUMULATIVE  PROBABILITY DISTRIBUTION  OF
       ACHIEVING REMOVAL PERCENTAGES GREATER
       THAN OR EQUAL TO A GIVEN VALUE                 91

62     CHLORINE DEMAND OF PLANT EFFLUENT              95

63     LIME USAGE  DURING REGENERATION STUDIES        96

64     IRON INVENTORY IN REGENERATED
       CARBON  SLURRY                                 107

65     INERTS  BUILDUP IN REGENERATED CARBON         109

66     JAR TESTS ON ONCE REGENERATED
       CARBON  - BATCH A                              112

67     JAR TESTS ON TWICE REGENERATED
       CARBON  - BATCH A                              113

68     JAR TESTS ON THREE TIMES
       REGENERATED CARBON - BATCH A                  114

69     JAR TESTS ON FOUR TIMES
       REGENERATED CARBON - BATCH A                  115

70     JAR TESTS ON ONCE AND TWICE
       REGENERATED CARBON - BATCH C                  116

71     JAR TESTS ON THREE TIMES
       REGENERATED CARBON - BATCH C                  117

72     JAR TESTS ON FOUR TIMES
       REGENERATED CARBON - BATCH C                  118

73     JAR TESTS ON FIVE AND SIX TIMES
       REGENERATED CARBON - BATCH C                  119

74     JAR TESTS ON SEVEN TIMES
       REGENERATED CARBON - BATCH C                  120

75     ALUMINUM BUILDUP IN REGENERATED  CARBON       123

76     ACID USAGE  DURING REGENERATION STUDIES       124

77     EFFECT  OF SLOWDOWN RATE ON TREATMENT
       COSTS FOR A 10 MGD PLANT                      132
                               IX

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                            TABLES

NO.                                                 PAGE

 1    DIURNAL WASTEWATER  CHARACTERISTICS AT
      ALBANY SITE DURING  DRY WEATHER                 28

 2    AVERAGE WASTEWATER  CHARACTERISTICS AT
      ALBANY SITE DURING  1971 PILOT OPERATIONS       32

 3    OPERATIONAL DATA DURING STORM FLOWS            37

 4    PLANT OPERATIONAL DATA FOR  1971
      STUDIES USING VIRGIN  CARBON                    61

 5    PLANT OPERATIONAL DATA FOR  DIURNAL STUDIES     62

 6    PLANT PERFORMANCE DATA DURING 1971
      OPERATIONS USING VIRGIN CARBON                 63

 7    PILOT PLANT PERFORMANCE AT  LOW CARBON DOSES    93

 8    REGENERATED CARBON  PERFORMANCE COMPARISON      98

 9    FLUIDIZED BED-FURNACE OPERATING  CONDITIONS    102

10    SIEVE ANALYSES OF FLUIDIZED BED  SAND          105

11    ALUMINUM MASS BALANCE SUMMARY                 122

12    STACK SAMPLING DATA                           126

13    CARBON MASS BALANCE SUMMARY                   128

14    SIEVE ANALYSIS OF FLUIDIZED BED  SAND
      COLLECTED WITH REGENERATED  CARBON              130

15    SYSTEM DESIGN PARAMETERS                       135

16    CAPITAL COST ESTIMATES  FOR  10 MGD
      MUNICIPAL WASTEWATER  AND  STORM WATER
      TREATMENT PLANTS                               136

17    SYSTEM OPERATING PARAMETERS                   137

18    OPERATING COST ESTIMATES  FOR 10  MGD
      MUNICIPAL WASTEWATER  AND  STORM WATER
      TREATMENT PLANTS                               138

19    TOTAL COSTS FOR 10  MGD MUNICIPAL WASTE-
      WATER AND STORM WATER TREATMENT  PLANTS        139

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                          SECTION XI

                          APPENDIX A



LABORATORY STUDIES

   GENERAL

   CARBON STUDIES

   TABLE A-l:   COMPOSITION OF HIGHLAND SEWAGE

                 BENCH SCALE SYSTEM
FIGURE A-l

FIGURE A-2:


FIGURE A-3


FIGURE A-4


TABLE A-2:
                 EFFECT OF  CARBON CONCENTRATION
                 ON  EQUILIBRIUM COD

                 EFFECT OF  CARBON CONCENTRATION
                 ON  EQUILIBRIUM TOC

                 EFFECT OF  CONTACT TIME
                 ON  TOC REMOVAL

               COMPARISON  OF VARIOUS
               CARBONS - CONTACT TESTS
   BENTONITE  PROCESS  DEVELOPMENT

   TABLE A-3:   COMPARISON OF VARIOUS
                CARBONS - JAR TESTS
   FIGURE A-5
             EFFECT  OF  BENTONITE CONCEN-
             TRATION ON EFFLUENT QUALITY
   TABLE A-4:   BENCH SCALE SYSTEM OPERATIONAL
                DATA - TUBE SETTLER

   TABLE A-5:   UPFLOW CLARIFIER OPERATING DATA

   ALUM PROCESS PRELIMINARY INVESTIGATIONS

   CARBON REGENERATION

   FIGURE A-6:   EFFECT OF ALUM DOES ON COD
                 AND TURBIDITY REMOVAL

   TABLE A-6:   UPFLOW CLARIFIER SYSTEM -
                ALUM PROCESS PERFORMANCE
 PAGE

  145

  145

  145

146-147

  148


  150


  151


  152


  153

  154


  155


  156


  157

  159

  160

  160


  161


  162

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(APPENDIX  A Continued)
   TABLE A-7:   TUBE SETTLER SYSTEM - ALUM PROCESS    163
   TABLE A-8:   ANALYSIS OF REGENERATED
               CARBON MIXTURES

   ALUM RECOVERY

   POLYELECTROLYTE SCREENING STUDY

   FIGURE A-7:   CAPACITY RECOVERY OF BATTELLE-
                COLUMBUS REGENERATED CARBON-ALUM
                PROCESS

   FIGURE A-8:   CAPACITY RECOVERY OF BATTELLE-
                COLUMBUS REGENERATED CARBON-
                BENTONITE PROCESS

   FIGURE A-9:   CAPACITY RECOVERY OF FMC
                REGENERATED CARBONS

   TABLE A-9:   JAR TEST RESULTS WITH
               REGENERATED CARBONS
   FIGURE A-10;


   FIGURE A-ll:


   TABLE A-10:
 EFFECT OF pH ON ALUMINUM
 RECOVERY

 ACID REQUIREMENT VERSUS pH-BCL
 CARBON-ALUM MIXTURE

FLOCCULATION PERFORMANCE OF
VARIOUS POLYELECTROLYTES
   TABLE A-ll:   EFFECT OF DOSE ON POLYELECTRO-
                LYTE PERFORMANCE - ALUM SYSTEM

   ALUM PROCESS OPTIMIZATION

   TABLE A-12:   EFFECT OF POLYELECTROLYTE DOSE
                ON BENCH SCALE PERFORMANCE
165

166

166



167



168


169


170


171


172


173


174

175


176

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                         SECTION I


                        CONCLUSIONS
A physical-chemical process utilizing powdered activated
carbon for the treatment of sanitary and combined sewage has
been successfully demonstrated on the 100,000 gal/day scale
at Albany, New York.  Carbon regeneration in a fluidized
bed furnace and alum recovery from the'calcined sludge have
also been demonstrated as has been reuse of the reclaimed
chemicals.  This demonstration project has established the
technical and economic feasibility of the process for both
sanitary and combined sewage treatment.   On the basis of
laboratory studies and the pilot plant demonstration, the
major conclusions listed below were drawn.

LIQUID TREATMENT PROCESS

     •  A process using powdered activated carbon, alum and
        a high molecular weight anionic polymer is highly
        effective in treating both sanitary and combined
        sewage.

     •  A carbon contact time of 5-10 minutes prior to
        hydrous aluminum oxide precipitation is required
        in order to insure consistently high treatment
        efficiency.

     •  A total carbon contact time of less than 15
        minutes is required for equilibrium removal of
        sorbable organics.

     •  The carbon dose can be adjusted to effect the
        degree of sorbable organic removal required.

     •  A residual, nonadsorbable fraction ranging from
        10-20 mg/1 BOD and 20-50 mg/1 COD existed at times
        in the Albany sewage.  This fraction could not be
        removed at activated carbon doses as high as
        1000 mg/1.

     •  A carbon dose of 500-600 mg/1 was required to
        produce a high quality effluent from the municipal
        sewage treated.

     •  It was possible to reduce the carbon dose to 200
        mg/1 during the nighttime hours at the Albany site
        without affecting effluent quality.  Decreasing the

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   carbon dose in this manner during that portion of
   the day when the sewage has a low soluble organic
   content can greatly reduce operating costs without
   sacrificing treatment efficiency.

a  An average carbon dose of 500 mg/1 achieved
   tertiary levels of treatment in the case of com-
   bined sewage during pilot operations.  Jar test
   data indicate that the required carbon dose to
   achieve these levels is less than 400 mg/1.

«  Alum  [A12(S04)3-18H20] and polyelectrolyte require-
   ments were 200 mg/1 and 2.0 mg/1, respectively for
   both sanitary and combined sewage treatment.

«  Lime  [Ca(OH)2]  requirements when reclaimed alum was
   used in the treatment process averaged 190 mg/1
   during the Albany, New York demonstration.  It should
   be possible to reduce the lime requirement to 150
   mg/1 or less in an actual operating plant.

*  Tube settling contributes to minimizing process
   detention time.  However, conventional sedimentation
   can be employed in the system if a longer process
   detention time is acceptable.

»  The tube settler operated effectively at a hydraulic
   loading of 2880 gpd/ft2.

®  Efficient filtration was  accomplished at filter
   loading rates in excess of 4 gpm/ft2.

»  Filtration provides an added degree of reliability
   which is essential for a  municipal waste treatment
   plant and therefore, should be included if the
   process is to be employed in this manner.  On the
   other hand, if a system is designed to operate
   during periods of combined overflow only and a
   certain amount of solids  carry-over in the effluent
   is acceptable,  filtration may not be necessary.

«  The powdered activated carbon treatment process
   can accommodate wide fluctuations in effluent
   composition.

*  The treatment system lends itself to a high degree
   of automation.

«  During periods  of storm flows it should be possible
   to adjust chemical feed rates automatically on the
   basis of influent flow rate.
                         — 2 —

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     «  Turbidity can be used as an index to predict
        changes in other influent parameters during periods
        of storm flows.   Thus, it may be feasible to adjust
        the carbon dose during a storm on the basis of
        turbidity.

     •  Treatment of raw and combined sewage can be
        accomplished in a total time of 50 minutes or less.
        This short detention time leads to a small land
        area requirement for the treatment system.

     »  The powdered activated carbon treatment process
        described in this report is free of the hydrogen
        sulfide problem associated with physical-chemical
        systems utilizing granular activated carbon.

     ®  The process can be operated on an intermittent
        basis with a negligible time requirement for
        startup if chemical feed stocks are maintained.

     «  The treatment process is highly reliable.

     «  Average removals in excess of 94 percent COD, 94
        percent BOD, and 99 percent suspended solids were
        consistently achieved in treating combined sewage.

     «  Average BOD, COD, suspended solids and turbidity
        levels in the pilot plant effluent from the
        sanitary sewage treatment operations were 17 mg/1,
        36 mg/1, 5 mg/1, and 0.6 JTU, respectively.

     «  In characterizing a waste stream or in shaking down
        a new plant, frequent sampling must be carried out
        in order to detect rapid fluctuations in waste
        stream composition.

     »  Physical-chemical treatment of raw municipal waste
        streams in some instances will produce tertiary
        levels of treatment while in others only secondary
        levels can be achieved.  Each waste stream must be
        examined on a case-by-case basis to determine the
        level of BOD removal which can be achieved-

SLUDGE HANDLING

     •  Carbon sludge should represent 1-2 percent of the
        plant flow in a full-scale facility.
                              -3-

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     •  A product containing 22 percent solids can be
        obtained from direct centrifugation of the
        carbon sludge.

     •  A conditioning polymer is required to achieve 95
        percent capture in the centrifuge.

     •  The required conditioning polymer dose for fresh
        sludge is 1-2 Ibs/ton dry solids.  Sludge aged
        for 2-3 days required a conditioning polymer dose
        of up to 4 Ibs/ton dry solids to achieve 95 percent
        capture in the centrifuge.

CARBON REGENERATION

     •  Powdered activated carbon can be successfully
        regenerated in a fluidized bed furnace.

     •  Satisfactory regeneration can be achieved at a
        temperature of 1250°F with a stack gas oxygen
        concentration of less than 0.5 percent.

     •  After 6.7 regenerations,  the regenerated carbon is
        as effective as virgin carbon in removing organic
        matter from raw sewage.

     •  Average carbon losses per regeneration cycle were
        9.7 percent.

     «  Hearth plugging problems  during the pilot plant
        operations resulted from  corrosion of the recycle
        gas system.   Such corrosion problems can be pre-
        cluded easily in design of a full scale  system.

     •  A high initial  buildup of inert materials in the
        regenerated carbon during the first cycle regenera-
        tions is believed to have resulted from  causes
        external to the regeneration system.  Installation
        of a grit chamber in the  treatment system should
        guard against high fluctuations in inert material
        buildup in the  regenerated product.

     «  Inert material  buildup averaged 2.9 percent per
        cycle during the pilot plant operations.

     «  Sand carryover  from the fluidized bed furnace is
        believed to represent the most significant fraction
        of this buildup.

     •  Minimum operating costs are achieved with a five
        percent blowdown of carbon and inerts.
                              -4-

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        Classification of the carbon and inerts would result
        in less carbon lost to blowdown and thus a reduction
        in operating costs.

        Stack gases from the regeneration furnace should not
        present significant air pollution problems.
ALUM RECOVERY
     •  Approximately 91 percent of the aluminum can be
        recovered by acidification of the carbon-alumina
        slurry to pH 2 with sulfuric acid after thermal
        regeneration of the carbon sludge.

     •  Acidification of the carbon-alumina slurry dissolves
        inerts in addition to alumina.  These dissolved
        solids are discharged in the plant effluent and thus
        the solids buildup in the reclaimed chemicals is
        reduced.

     »  Sulfuric acid requirements for alum recovery were
        0.6 Ibs H2SC>4/lb of carbon for the pilot operations.
        A reduction to 0.5 Ibs H2SC>4/lb of carbon appears
        feasible.
                              -5-

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                    SECTION II
                 RE COMMEN DATION S

•  As a result of the successful laboratory studies
   and pilot plant demonstration, efforts should
   proceed toward a full-scale demonstration of the
   powdered activated carbon treatment process.
•  The powdered carbon treatment process should be
   demonstrated on a large scale basis for treatment
   of both raw and combined sewage.

•  Design parameters for conventional sedimentation
   should be developed.

•  An effort should be initiated to define the upper
   limit of loading of the tube settler without solids
   carryover.

»  The necessity of stack gas recycle should be
   examined since elimination of the stack gas recycle
   stream would reduce capital costs.

•  A reliable and accurate analytical method for
   determining the spent carbon content of sludge
   should be developed.

•  If the powdered activated carbon process is to be
   used as an advanced waste treatment process for the
   treatment of raw sewage, it would be desirable to
   develop a method to remove phosphorus from the
   reclaimed alum.  This would provide the added
   dimension of phosphate removal in the treatment
   process.

*  The composition of the nonadsorbable organic
   fraction should be determined and methods for its
   removal explored.

•  An efficient classification method for separating
   sand from regenerated carbon should be identified
   to reduce total blowdown and carbon losses.

9  Further investigation of the usefulness of turbidity
   as an index of solids and organic loadings during
   storms should be pursued with a view towards auto-
   mation of carbon and chemical feed rates in response
   to turbidity monitoring signals.
                         -7-

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                        SECTION III
                        INTRODUCTION


The problem posed by combined sewer overflows is
well documented.  In 1967, it was estimated that $48
billion would be required to eliminate these overflows by
installing separate collection systems for sanitary wastes
and storm water(!).  This estimate did not include the
monetary loss which would be experienced by commerce and
industry as the streets through the centers of major cities
were torn up for installation of the separated systems.  In
addition to economics, the possibility of separation of all
sewers, particularly in areas of high population density,
was remote.  Even if complete separation were accomplished,
this measure would not be entirely satisfactory since storm
water runoff is, itself, often severely polluted, particu-
larly in highly urbanized, areas(2,3,4).  jn fact, the
pollutional effect of surface drainage water can be so
significant that it will, in many cases, be necessary to
treat storm runoff before it is allowed to reach receiving
waters(4) .

Recognizing the tremendous problems associated with sewer
separation, the Storm and Combined Sewer Pollution Control
Branch of the Water Quality Office embarked on a program
to seek alternatives to this measure.  They estimated that
the development of alternative means of treatment could
conceivably reduce this cost by two-thirds.

Therefore, as part of the Water Quality Office program,
Contract No. 14-12-519 was negotiated with Battelle-Northwest
to develop, through laboratory experimentation and pilot
plant demonstration, a novel physical-chemical process for
treatment of combined storm and sanitary sewage.

The treatment process was developed with the following
goals:

     «  The quality of the effluent should be comparable
        to that routinely discharged from a secondary
        sewage treatment plant.

     •  Short detention times are mandatory due to the
        high flow rates likely to be encountered and the
        undesirability of allocating large land areas
        for treatment of combined sewage.

     «  The process must be amenable to intermittent
        operation with a minimum time requirement for
        startup.
                              -9-

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     9  Treatment of combined sewage by such a process
        must be economically feasible.

The developed process, as outlined in Figure 1, involves
contacting raw or combined sewage with powdered activated
carbon to effect removal of dissolved organic matter.  An
inorganic coagulant, alum, is then used to aid in subsequent
clarification.  Addition of polyelectrolyte is followed by
a short flocculation period.  Solids are separated from the
liquid stream by gravity settling, and the effluent is then
disinfected and discharged or can be filtered prior to dis-
infection.

Bench scale laboratory experiments and pilot studies  indi-
cated that a 30-45 minute overall detention time is required.
A ten-minute contact time prior to flocculation is necessary
for good organic removal.  Floe with excellent settling
characteristics is consistently produced.  This, coupled
with highly efficient tube settling, leads to the very short
process detention time.
Carbon sludge from the treatment process is thermally re-
generated by a fluidized bed process.  Alum is recovered by
acidifying the regenerated carbon-aluminum oxide mixture to
pH 2 with sulfuric acid.  This reclaimed alum is then reused
in the treatment process.  A pH adjustment, accomplished
with a lime slurry, is required to raise the pH to 6.5-7.0
for aluminum hydroxide precipitation when reclaimed alum
is recycled.

A nine-month laboratory study which is described in Appendix
A and elsewhere(5) indicated that the process goals could be
met.  In  addition, the laboratory phase of the program
demonstrated that the treatment process could be highly
effective for raw sewage.  Consequently, a 100,000 gpd
mobile treatment plant  (Figure 2) was designed and con-
structed.

Following construction of the mobile pilot plant, it  was
operated  for a one-month shakedown at Richland, Washington.
After minor equipment alterations were made, the process
performed as well or better than anticipated from the
laboratory study.  Although this operation at Richland was
primarily for shakedown purposes, a limited amount of per-
formance  data was obtained.  Treating raw municipal wastes,
TOC^removals averaged better than 90 percent while suspended
solids removals averaged better than 95 percent.  Product
water turbidities were consistently below 2 JTU.  The resul-
tant sludges were dewatered to 20 percent solids in a contin-
uous solid bowl centrifuge without any preconditioning or
supplemental thickening.
                             -10-

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      MAKEUP       pH
      ALUM  &   ADJUSTMENT
     POWDERED    (LIME)
     ACTIVATED
      CARBON
RAW
SEWAGE
OR
COMBINED'
SEWER
OVERFLOW
POLYMER
                                                      FILTRATION
     RECYCLED
                H2S04 TO pH 2
M &
)ERED
.BON
\
f
t

FLUIDIZED
BED
FURNACE

                                     SLUDGE
                                   DEWATERING
      INERT
       ASH
     SLOWDOWN
                    FIGURE  1.   PROCESS  FLOW SHEET

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FIGURE 2.  MOBILE  PILOT PLANT

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Upon completion of the shakedown operation, the mobile pilot
plant was shipped to Albany, New York, where it was operated
from mid-June through October 1971.  Since the pilot plant
was not designed for cold weather operation, it was shut down
for the winter months.  Operations were resumed in early
April of 1972 and continued through the month of June of that
year.  This report describes the results of the pilot plant
demonstration in Albany.
                             -13-

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                         SECTION IV


                  PILOT PLANT DESCRIPTION


The pilot plant is composed of two major systems:  a liquid
treatment system and a carbon regeneration facility.

TREATMENT SYSTEM

The liquid treatment system is housed, almost entirely, in
a forty-foot mobile trailer van.  A schematic diagram of the
process flowsheet is given in Figure 3.  The major compon-
ents are

     •  Surge Tank
     «  Pipe Reactor and Static Mixers
     •  Chemical Addition Equipment
     «  Flocculation Chambers
     «  Tube Settler
     »  Tri-media Filter
     »  Centrifuge

It is designed for a nominal capacity of 100,000 gal/day.
Carbon, alum, and polyelectrolyte are added in a pipe reactor,
providing rapid mixing of the chemicals, which preceeds
flocculation followed by separation via a tube settler.
Clarified effluent is chlorinated and released with the
option of routing through a gravity filter prior to chlorin-
ation.  Sludge is dewatered in the centrifuge.

The system is designed for maximum operational flexibility
and includes turbidity, pH and flow monitoring instruments.

Sanitary or combined sewage is pumped from a sewer to a surge
tank, screened and then pumped to a six-inch diameter
stainless steel pipe reactor.  The pipe reactor consists
of 62 sections of 7"4" pipe arranged in an eight by eight
array.  The pipe centers are located at the apexes of equi-
lateral triangles.  This arrangement allows for one pipe
elbow section to be connected at six locations while rotating
through a 360° circle.  Connections between straight pipe
lengths and 180° returns are made with quick disconnect
couplings.

The total pipe reactor length of 560 feet will allow a
detention time of ten minutes at a flow rate of 75 gpm.
Chemical feed connections are provided at various locations
along the pipe reactor as illustrated in Figure 4 with
                             -15-

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CTl
1
                    LIME
                       ri
ACIDIFIED ALUM-
CARBON  SLURRY
FROM  FURNACE


     DEWATERED
     SLUDGE
     TO FURNACE
-POLYELECTROLYTE

        JL_O	a.
                                                              HYPOCHLORITE
t
L


1
C
3
:
5
;
i i
i
FLOCCULATOR
i
                                                           SLUDGE  STORAGE
                                         FILTERED
                                         WATER
                                         STORAGE
                                     'STORAGE TANK
                    FIGURE  3.   SCHEMATIC FLOWSHEET OF MOBILE PILOT PLANT

-------
                                                       f
FIGURE 4.  CHEMICAL  INJECTION POINT IN PIPE  REACTOR
                        -17-

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helical static mixers located after each chemical  injection
point.  These static mixers assure rapid, effective  chemical
mixing.  Powdered activated carbon and alum  are  added  at  the
head end of the pipe reactor, lime is added  to adjust  the pH
approximately 280 feet downstream and finally, polyelectro-
lyte is added at the end of the pipe reactor.

After polyelectrolyte addition, the treated  influent can  be
divided into one, two or three parallel streams.   Each
stream enters a 400 gallon flocculator.  At  25 gpm per
flocculator, nominal detention time is sixteen minutes.

Flocculator effluent leaves through a six-inch valve and
enters the tube settler via an increasing cross-sectional
area channel which keeps the flow velocity below one-foot
per second to minimize break up of floe.  The tube settler
contains 25 sq. ft. of steeply (60°) inclined tubes.  Separated
sludge is pumped to a 3200 gallon storage tank prior to
dewatering.  Tube settler effluent can be chlorinated  and
discharged directly or can be filtered prior to disinfection.
Filtration is accomplished in a 16 sq. ft. tri-media filter.
The filter contains 5 in. of 40 x 80 mesh garnet sand, 9  in.
of 20 x 40 mesh quartz sand, and 16.5 in. of 10 x  40 mesh
anthrafilt.

^A six-inch solid bowl centrifuge is used to dewater  sludge
which is then stored in a holding tank and subsequently
pumped to the carbon regeneration facility.  Centrate  from
the dewatering operation and filter backwash water are
returned to the surge tank for recycle through the treatment
system.

REGENERATION FACILITY

The fluidized inert sand bed unit of the regeneration  facility
is 36 in. I.D., refractory lined, and self supported.  As
illustrated in Figure 5, this unit consists of three main
sections:  a firebox housing the burner 30 in. I.D.  x  20  in.
high, a bed section containing inert sand 27 in. I.D.
bottom, 36 in. I.D. top x 60 in.  high and a freeboard  36  in.
I.D. x 72 in. high.

Combustion of propane gas takes place in the firebox which
is also the point of injection of recycling gases  to main-
tain a 2,000°F atmosphere.   The hot gases pass through ver-
tical holes in a brick hearth fluidizing the inert sand
bed.   Carbon sludge at approximately 78~percent moisture
is injected into the 1250°F turbulent bed where rapid  heat
transfer is obtained between gases and materials.  The
mixture of steam,  combustion products, and regenerated
                             -18-

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  WATER OR
  RECYCLE GAS
OBSERVATION  PORT
AND SAND  FEED  BIN
                                           SAND LFVFL
                                           FLUIDIZED
                                             SLURRY
                                           INJECTION
                                              PORT
  DOORS
  SAND C L E A N 0 UT
 RECYCLE GAS INLET
        FIGURE  5.   FLUIDIZED BED  REGENERATION  UNIT
                              -19-

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carbon rises to the freeboard area and exits near  the  fur-
nace top on the side at 1200°F to a venturi scrubber and
cyclonic type separator.  Exhaust gases at 150-200°F are
vented to the atmosphere through a scrubber stack  with a
portion being recycled to the firebox.  The regenerated
carbon slurry from the scrubber is passed through  a 60 mesh
screen to remove large sand particles carried over from the
fluidized bed.  During the 1972 operation, a small settling
chamber, three inches deep by one foot square, was installed
ahead of the screen.  Most of the larger sand particles were
captured in this chamber, thus reducing the load on the screen
and eliminating the need for frequent cleaning of  the  screen.
After passing through the 60 mesh screen, the slurry was
collected in storage tanks.  Water for the venturi scrubber
was continuously decanted from the storage tanks at 6-12 gpm
and recirculated.

The fluidized bed is suitably lined to produce a maximum skin
temperature of 150-200°F, while a bed temperature  of approxi-
mately 1500°F is maintained.  The shell itself is  of steel
construction.  The whole system is pressurized (windbox,
bed, freeboard) such that the summation of pressure drop
through the fluidized bed and scrubbing system will be less
than the pressure developed by the turbo-blowers.  The
fluidized bed is provided with necessary access port,  obser-
vation port, sand inlet, sampling ports, sand clean-out,
thermocouples, pressure tap connections, feed inlets and
auxiliary propane gas gun.

Once furnace operation is begun, its control is automatic.
Combustion air, recycle gas, propane and carbon sludge flow
rates are initially set manually to achieve the desired
temperatures, 02 level, and bed velocity.  Once set, the bed
temperature is maintained automatically by varying the com-
bustion air flowrate.  (The propane flow changes proportion-
ately with the combustion air flow to maintain a relatively
constant 02 level.)

After collection, the regenerated carbon slurry is acidified
to pH 2 with sulfuric acid in order to reclaim the alum
before reuse in the system.

A schematic diagram of the carbon regeneration system  is
presented in Figure 6.   Figures 7 and 8 are two views  of the
regeneration furnace in place at the Albany site.
                             -20-

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1
ho
H-
J
           DEWATERED
           SLUDGE
             PROPANE
           COMBUSTION
           AIR
                                                                        SCRUBBED
                                                                        STACK GAS
                                                                                         FEED
                                                                                          TO
                                                                                        TRAILER
MAKEUP ALUM

MAKEUP CARBON
                                       REGENERATION
                                         FURNACE
                         FIGURE 6.   REGENERATION SYSTEM  SCHEMATIC  FLOWSHEET

-------
i
M
                                  WATER POLLUTION CONTROL RESEARCH
                     FIGURE  7.   PILOT PLANT IN OPERATION AT ALBANY SITE

-------
U)
1
                            FIGURE 8.  FLUIDIZED BED CONTROL PANEL

-------
                         SECTION V


                     DEMONSTRATION SITE


SITE DESCRIPTION

The demonstration site was located in the 400 block of South
Pearl Street in Albany, New York.  Raw or combined sewage
was drawn from a 91 inch combined sewer,- which serves the
Island Creek District in Albany.  A site location map showing
the demonstration site and drainage area is given in Figure 9.
This drainage area is about 550 acres in size with a popula-
tion of approximately 10,000.  Perhaps 10-15 percent of the
area is comprised of small commercial businesses with the
remainder being mainly residential in nature.  No light or
heavy industry is located in the drainage area.

The average annual precipitation in Albany varies between
35 and 37 inches with the heaviest rainfall usually occurring
in June, July, and August.

WASTEWATER FLOW AND CHARACTERISTICS

Average dry weather flow  (DWF) in the 91 inch trunk sewer
at the demonstration site was measured as 720 gpm.  Average
minimum daily flow which occurred at approximately 0500 was
610 gpm and the average maximum daily flow of 820 gpm
occurred between 1000-1200.  Figure 10 contains typical
diurnal flow data for the Albany site.

The physical and chemical characteristics of the raw waste-
water at the site were observed to be highly variable.
Initially, grab samples were obtained at two-hour intervals
for several twenty-four hour periods and analyzed for various
constituents.  During the 1972 operation, samplers were in-
stalled to collect hourly composite samples.  These data  are
presented in Table 1 and Figures 11-13.  Daily averages for
the maximum, minimum, and average day during the pilot
operations are presented in Table 2.

An unusually high COD peak was observed to occur frequently
at about 1400 as indicated in Figure 11.  Such a high COD
peak was unexpected for a purely residential area.  Moreover,
the time of occurrence is also somewhat unusual.  The source
of this frequent high COD slug was not identified.
                              -25-

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                                                              ISLAND CREEK DRAINAGE AREA
                                                                  ALBANY, NEW YORK
CJ1
 I
                                                                                                           DEMONSTRATION SITE
                                                                                                                                HUDSON

                                                                                                                                RIVER
                 FIGURE-9.    ISLAND  CREEK  DRAINAGE AREA  AND  DEMONSTRATION  SITE  LOCATION

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                      TABLE  1
DIURNAL WASTEWATER CHARACTERISTICS  AT ALBANY SITE
               DURING DRY WEATHER
Time
of Day
0800
1000
1200
1400
1600
1800
2000
2200
2400
0200
0400
0600
NOTE :
Suspended
Solids
(mg/1)
370-63
188-13
273-104
179-15
287-27
149-13
500-47
159-16
304-34
135-17
420-76
172-17
247-54
130-16
322-10
123-14
198-33
89-18
246-14
65-17
62-12
29-14
206-11
68-14
COD
(mg/1)
778-138
288-18
616-175
381-19
472-206
362-18
5200-165
713-20
575-95
324-22
572-208
325-20
390-106
251-20
460-82
218-19
215-13
132-22
292-32
90-24
305-25
67-22
979-25
162-21
BOD
(mg/1)
108-54
83-11
390-80
162-14
230-62
123-10
678-58
162-11
300-38
134-15
200-74
129-16
151-57
100-14
160-48
93-12
120-24
75-12
77-12
38-13
111-12
27-13
110-16
41-12
Total P
(mg/1)
42.6-10.0
27.1-13
60.0-20.0
35.8-16
49.8-18.0
29.4-13
64.5-12.6
28.7-16
137-10.0
27.3-17
31.0-16
22.3-16
36.6-6.6
20.0-17
26.4-4.0
15.0-14
17.3-2.7
11.6-17
15.6-2.7
7.4-13
18.0-3.3
8.5-12
29.9-3.9
12.6-14
Turbidity
(JTU)
150-34
80-13
220-61
100-13
148-43
86-14
200-31
82-14
150-31
85-16
274-25
105-17
144-33
77-13
123-27
51-11
64-13
32-13
78-9
21-12
42-1
17-12
150-3
44-12
Numbers for each time period represent: fhiah value - low vali
                                  S average -no. of samples?
                   -28-

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l
to
               150
               100
            o
            oa
                50
                                                       • BOD

                                                       O COD
                   _L
                             I
                  0800     1200
                                              I
                  _L
 _L
                                       800
                                                                           600
                                       400  o
                                            CJ
                                                                           200
1600    2000     2400
      TIME OF DAY
0400     0800
             FIGURE 11.   AVERAGE DIURNAL BOD AND  COD FLUCTUATION AT ALBANY  SITE

-------
            100 -
          CQ
          ce
                         O TURBIDITY
                         A SUSPENDED  SOLIDS
             20 .
               0800      1200     1600     2000    2400
                                       TIME OF DAY
0400
                                                                       - 200
                                                                       - 150
           - 100
                                                                            GO
                                                                            Q
                                                                            O
                                                                            GO
                 UJ
                 O
                                                                            D_
                                                                            GO
                                                                       -  50
0800
FIGURE 12.  AVERAGE DIURNAL SUSPENDED SOLIDS AND TURBIDITY FLUCTUATION AT ALBANY SITE

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l-1
l
            40
            30
0_
co
            20
            10
      0800      1200
                                    1600      2000
                                          TIME OF DAY
2400      0400
0800
               FIGURE 13.  AVERAGE DIURNAL PHOSPHATE FLUCTUATIONS  AT  ALBANY SITE

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                                                          TABLE 2
                                    AVERAGE WASTEWATEH CHARACTERISTICS AT ALBANY SITE
                                                DURING 1971 PILOT OPERATIONS
                                         Total
                                                            Volatile
         COD  BOD  Turbidity
                            2  Total   Volatile  Suspended  Suspended  Settleable
                               Solids   Solids    Solids     Solids      Solids


I
U)
NJ
1

Maximum
Minimum

Average

No. Days
483
60

276

42
159
47

104

37
315
24

54

43
533
320

419

18
268
144

193

16
668
43

130

45
150
11

69

16
4.0
1.0

2.8

11
All units mg/1 except as noted
Units are JTU
Organic
                                                                                                                  Total
                                                                                    NH3-N  Nitrogen NO2-N  NO3-N  PO4

                                                                                      55      25     0.2    1.0     57

                                                                                      12       7.6   0.002  <0.1     12.6

                                                                                      22      11.3   0.06   0.3     24.9

                                                                                      12      12     12     9       13
Units are ml/1 after 1/2 hr.  settling

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                         SECTION VI


                TREATMENT SYSTEM PERFORMANCE

GENERAL

All analytical procedures were carried out in accordance
with Standard Methods'    unless otherwise noted.  During
the course of the field work, most of the analytical work
was subcontracted to Environment One Corporation of Schenec-
tady, New York.   The New York State Department of Environ-
mental Conservation provided significant analytical support
to this program, especially in characterizing the waste stream
at the demonstration site.

Jar tests were carried out routinely in support of the pilot
plant activities.  The general procedure involved addition
of the desired quantity of carbon slurry to one liter of
sewage and then adjustment of the pH to 4 with sulfuric acid
prior to addition of 200 mg/1 of alum.  Samples were then
subjected to a ten minute rapid mix whereupon the pH was
adjusted to 7 with Ca(OH)2-  Rapid mixing was continued for
an additional five minutes before addition of 2 mg/1 of
polyelectrolyte.  Following an additional half minute of rapid
mixing, the sample was flocculated at 10 rpm for five minutes
and was then allowed to settle for twenty minutes.  Super-
natant samples were decanted for analytical determinations.
In most instances, these samples were analyzed for BOD and
COD directly.  Those cases in which samples were filtered
through 0.45y membrane filters are identified in the text
as "soluble" BOD and COD determinations.

PLANT OPERATION

During the course of the pilot plant studies , both virgin
carbon and regenerated carbon were used in the treatment
system.  When virgin carbon  (first cycle) was employed for
any run in the pilot plant, alum was added to the carbon
slurry (6 percent carbon by weight) in a chemical feed tank
and the mixture was acidified to pH 2 with sulfuric acid
prior to use.  This simulated the conditions of a regenerated
carbon slurry which had been acidified to reclaim alum.
Injection of this acidified carbon-alum slurry into the raw
wastewater resulted in a pH of 3.5-4.

Careful control of the pH within the system was critical to
proper process performance.  The laboratory studies showed
that, in order to consistently achieve good flocculation,
it was essential to provide several minutes of carbon contact
                             -33-

-------
with the wastewater prior to formation of the hydrous
aluminum oxide.  In the pilot plant, this was achieved bv
maintaining the pH below 4 for the first five minutes of
contact and then adjusting the pH to 6.5-7 with a lime
slurry.  It was observed, in the course of the pilot
studies, that if the pH was allowed to rise above pH 4 within
the first few minutes, fine carbon particles were carried
over from the tube settler causing rapid filter plugging.
Moreover, under these conditions, the turbidity of the
filter effluent increased considerably.  A three percent
lime slurry was used to adjust the pH in the system.  Lime
feed was controlled automatically on the basis of pH.

Throughout the pilot operations, the alum [A12(804)3 -18H20]
dose was held constant at approximately 200 mg/1.  It was
determined that the flocculation-sedimentation process deteri-
orated considerably if the alum dose was reduced much below
the 200 mg/1 level.  On the other hand, the carbon dose
could be varied from 0-1100 mg/1 while maintaining the alum  dose
at 200 mg/1 with no serious effect on the flocculation-
sedimentation efficiency.

Two types of powdered activated carbon were used in the study:
Agua Nuchar  (product of WESTVACO) and Darco XPC  (product of
ICI America, Inc.).  Analyses showed Aqua Nuchar A to be
approximately 90 percent fixed carbon while the Darco product
contained only 70-80 percent fixed carbon.  Both carbons
performed comparably in the pilot studies at equal fixed
carbon doses.  The relatively low fixed carbon content of
the Darco XPC is not surprising since this is an unwashed
grade of lignite carbon.  After several adsorption/
regeneration cycles, the differences between this and a
washed grade of carbon may not be significant.  However, it
was decided to use the higher grade Aqua Nuchar A for the
bulk of the pilot operations.

Three different high molecular weight anionic polyelectrolytes
were used in the pilot study:  Atlasep 2A2  (product of ICI
America, Inc.), Decolyte 930 (product of Diamond Shamrock
Chemical Company), and Purifloc A-23 (product of Dow Chemical
Company).  All of these polymers were observed to produce
large,  rapidly settling floe particles.  Each of these poly-
electrolytes performed satisfactorily at a dose of 2 mg/1.

Initially,  high solids carryover from the tube settler was
observed when the system was operated at a flow rate greater
than 50 gpm.   It was determined that this problem was the
result  of poor flow distribution within the unit.  Subse-
quently,  a  new influent distributor was installed in the
tube settler and the unit performed well at the design flow
of 70  gpm.   This represents an overflow rate of 2880 gpd/ft2.
                              -34-

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Under these conditions, the turbidity of the effluent from
the tube settler was consistently <2 JTU.  Filter runs averaged
ten hours at a filter loading rate of 4.4 gpm/ft2.  Backwash
was initiated at a terminal head loss of approximately 10 psi.

Sludge withdrawal was accomplished by pumping the sludge
from the base of the two hopper bottoms of the pilot tube
settler.  Since there was no mechanical collection system in
the tube settler, it was necessary to withdraw the sludge
at a rate of approximately nine percent of the plant flow.
This sludge rapidly settled to 10-20 percent of its original
volume in the sludge storage tank.  Therefore, it is reason-
able to expect that in a large clarifier with a mechanical
scraper, sludge volume would be 1-2 percent of the plant flow.
However, the absence of a mechanical scraper in the tube
settler did cause an additional problem.  Channeling tended
to occur during sludge withdrawal even though the sludge
pump was operated on a 90 seconds on, 30 seconds off cycle
to minimize this problem.  Consequently, efficient withdrawal
of sludge was not accomplished and the tube settler tended to
fill with sludge after about 48 hours operation.  When this
occurred, solids tended to overflow from the tube settler and
onto the filter.  The only feasible means found to correct
this condition was to completely drain the tube settler prior
to continuing operations.  Once again, this problem should
not occur in a large clarifier or tube settler with a
mechanical scraper.

At no time during the operations was hydrogen sulfide de-
tected in the plant effluent.  Even after the system had been
idle for several days an H2S odor was generally not detected
in the closed process trailer.  However, in warm weather if
the system was not in operation and sludge was allowed to
remain in the tube settler for 2-3 days time, H2S was ob-
served to form.  In actual plant operation, the sludge age
should be nowhere near two days and thus hydrogen sulfide
should not be a problem.

The carbon sludge was readily dewaterable in a Bird six-inch
solid bowl centrifuge.  Dewatered sludge ranged from 20-35
percent solids at 70 percent capture with no conditioning
polymer.

Initial operation at a pool depth of 0.35 inch produced sludge
containing 26 percent solids.  This sludge was very viscous and
extremely difficult to pump to the regeneration facility.  In-
creasing the pool depth to 0.5 inch produced a much more
pumpable, 22 percent solids sludge.  It was found that rapid
mixing of the dewatered sludge reduced its viscosity render-
ing it much more easily pumped.
                             -35-

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Solids capture was found to be improved by treating the
sludge with the same polymer used in the waste treatment
process.  A polymer dose of 2 Ibs/ton dry solids increased
solids capture to greater than 95 percent.  Since no polymer
screening tests were conducted, it is expected that the 2
Ibs/ton dose can be reduced substantially by selection of
the proper conditioning agent.

It was found that as the sludge aged, the polymer dose required
for conditioning increased.  Sludge more than 2-3 days old
required polymer doses as high as 4 Ibs/ton to achieve the
same solids capture in the centrifuge.

COMBINED SEWAGE TREATMENT

The treatment system performed well during the course of
nine storm events which occurred during the summer and fall of
1971 and in the spring of 1972 at the Albany site.  These
storm events ranged in duration from 2 to 7 hours with the
total rainfall during a single event ranging from 0.05 to
1.13 inches.  Thus the combined sewage flows handled by the
treatment system are representative of a range of conditions
typical of the Albany area.

Operational data for the pilot treatment system during these
storms are given in Table 3.  Turbidity, suspended solids, COD,
and BOD data for the storms are presented in Figures 14-32.
Plant detention times (listed in Table 3) should be taken into
account when comparing effluent quality data with influent
waste composition in these figures.  Throughout the course
of all of these storms,  plant effluent turbidity rarely ex-
ceeded 1 JTU and effluent suspended solids ranged from <1-18
mg/1, while the influent suspended solids exceeded 8800 mg/1
at the peak of one storm.  Effluent COD, BOD, and suspended
solids averaged 23, 6.0, and 4.2 mg/1,  respectively.  This
represents average removals of 94 percent COD, 94 percent
BOD, and 99 percent suspended solids.  During the peak pollutant
loadings of these storms the effluent quality remained essentially
unaffected resulting in removals as high as 99 percent COD, 99
percent BOD, and 99.9 percent suspended solids.

Inspection of the data in Figures 20, 28, 30, and 32 reveals
that the greatest portion of the COD in the combined sewage at
the Albany site was insoluble.  However, these data also show
that the soluble fraction of the COD is of significant magni-
tude.  This suggests that although solids removal is perhaps
the most important factor in combined sewage treatment, it is
not sufficient to produce a high quality effluent.
                             -36-

-------
              TABLE 3
OPERATIONAL DATA DURING STORM  FLOWS
Date
7/13/71
7/19/71
7/29/71
9/16-17/71
5/2/72
5/16/72
5/16/72
5/16-17/72
Total
Rainfall
(inches)
0.39
0.55
0.30
0.46
0.20
0.05
0.15
0.45
Combined
Flow
Duration
2030-0200
1100-1600
1545-2000
2100-2215
2215-0100
0330-0730
0215-0430
0530-0730
2000-0230
Plant
Flow
(gpm)
42
70
50
40
75
40
40
40
40
Detention
Time
(minutes)
85
50
70
88
47
88
88
88
88
Carbon
Dose
Cmg/1)
1300
625
800
800
800
570
500
500
500
              -37-

-------
  240
  160
CO
Er  80
  200
  160
oo
o
00

Q
O.
00
  120
   80
   40
       CONDITIONS
DARCO XPC @ 1300
DETENTION TIME: 85 MIN
     o PLANT  INFLUENT

     • PLANT  EFFLUENT
                                          PLANT  EFFLUENT
                                             JTU
                                                        J
2030    2100
                           2200
                            TIME  OF  DAY
       2300
2400
          FIGURE 14.   STORM EFFECT ON TURBIDITY AND
                      SUSPENDED SOLIDS - 7/13/71
                            -38-

-------
I
U>
1000
 800
           600
           400
           200
                                                              I        i         r
                                                                CONDITIONS

                                                         DARCO XPC @ 1300 mg/fc
                                                         DETENTION TIME: 85 MIN
                                                          O PLANT INFLUENT

                                                          • PLANT EFFLUENT
                                            I
                                                                      I
                 2030     2100    2130    2200     2230
                                            TIME OF DAY
                                                 2300
2330
2400
                           FIGURE 15.  STORM EFFECT ON COD - 7/13/71

-------
CD
o;
  4000 -
   3000
   2000
   1000
                            "I	1	1	

                                    CONDITIONS

                             DARCO XPC @ 625 mg/S,
                             DETENTION TIME: 50  MIN
                                       O PLANT INFLUENT
                                   MAXIMUM  EFFLUENT
                                   TURBIDITY  <1  JTU
   8000
CD
E
ui
o
o
ut

o
LLJ
o
   6000
4000
   2000
                                   MAXIMUM  EFFLUENT
                                   S.S. <13
          1000    1200    1400    1600   1800    2000
                           TIME OF DAY
          FIGURE 16.   STORM EFFECT ON TURBIDITY AND
                      SUSPENDED SOLIDS - 7/19/71
                            -40-

-------
  700
  600
  500
  400
O
O
I        I       I
      CONDITIONS
DARCO XPC (a 625 mg/£
DETENTION TIME: 50 MIN
 O PLANT INFLUENT
 • PLANT EFFLUENT
  300
  200
  100
                                              _L
       1100    1200    1300   1400    1500
                          TIME OF DAY
                                    1600
1700
         FIGURE  17.   STORM  EFFECT  ON COD - 7/19/71
                            -41-

-------
D

CD
   500 -
   400
   300
   200
   100
	1	1	1	
      CONDITIONS

DARCO XPC @ 800 mg/X,
DETENTION TIME: 70 MI

 O PLANT INFLUENT

 • PLANT EFFLUENT
                                    PLANT EFFLUENT<1 JTU

                                  J	I	I	I
  1600
en
E
  1200
o
00
   800
   400
           1600    1630    1700    1730     1800    1830    1900
                             TIME  OF  DAY
          FIGURE  18.  STORM EFFECT  ON TURBIDITY AND
                       SUSPENDED SOLIDS - 7/29/71
                              -42-

-------
i
>£*
U)
          25
          20
          15
        CO
        •a;
        LU
          10
                                   CONDITIONS

                          DARCO XPC @ 800 mg/A
                          DETENTION TIME: 70 MIN
                             o PLANT  INFLUENT
                  1600
1700
    1800
TIME OF DAY
1900
2000
                    FIGURE 19.  STORM  EFFECT  ON  SETTLEABLE SOLIDS - 7/29/71

-------
   400
   300
1*  200
Q
O
CO

   100
     I       I        I
        CONDITIONS

DARCO XPC @ 800 mg/£
DETENTION TIME: 70 Mil

O PLANT INFLUENT

• PLANT EFFLUENT


                                                 _L
  1200h
  loooh
   800U
O PLANT  INFLUENT,  TOTAL

A PLANT  INFLUENT,  SOLUBLE

• PLANT  EFFLUENT
Q
O
O
   600h
   400h
   200h

            1600   1700   1800   1900
                          TIME OF DAY
           2000
2100
     FIGURE 20.  STORM EFFECT ON BOD AND COD - 7/29/71
                           -44-

-------
  4000
  3000
  2000
CO
CCL
  1000
 10,000
  8000
  6000
	I
o
I/O

o

a 4000

UJ
Q_
OO
rs

1/1 2000
              	1	1	1	T

                  CONDITIONS

              AQUA NUCHAR @ 800 mg/Ji
              DETENTION TIME:  115  MIN


               O PLANT INFLUENT


              EFFLUENT TURBIDITY <1 JTU
              EFFLUENT S.S. <
                                                    mg/£
      2300    2400
0100   0200    0300
        TIME OF DAY
0400   0500   0600
          FIGURE 21.   STORM EFFECT ON TURBIDITY AND

                      SUSPENDED SOLIDS - 9/13-14/71
                            -45-

-------
  160
  120 -
O
CO
    1	1
CONDITIONS
                               AQUA NUCHAR @ 800 mg/£
                               DETENTION TIME:  115 MI
                                O PLANT  INFLUENT

                                • PLANT  EFFLUENT
   40 -
   600 -
   500
   400
 CD
 E
 a
 o
   300
   200
   100
              I
      2300  2400    0100   0200   0300   0400
                            TIME OF DAY
          0500   0600
    FIGURE 22.  STORM EFFECT ON BOD AND COD  -  9/13-14/71
                             -46-

-------
  160
  120
   I       '


O PLANT INFLUENT

• PLANT EFFLUENT
03
Oi
   80
   40
       CONDITIONS

AQUA NUCHAR 0 800 mg/£
DETENTION TIME:
    BEFORE 2215 - 88 MIN
    AFTER 2215  - 47 MIN
  800
cr>
E
oo
O
  600
o
00

o 400
UJ
o
z:
LiJ

oo
=> 200
            2200
                2300
                 TIME OF DAY
        2400
0100
          FIGURE 23.  STORM EFFECT ON TURBIDITY AND

                      SUSPENDED SOLIDS  -  9/16-17/71
                            -47-

-------
  160
  120
Q
O
CD
   80
   40
  400
   300
en
£
   200
   100
                                         1 - .
                                          CONDITIONS
              mg/«.
                                   AQUA NUCHAR @ 800
                                   DETENTION TIME:
                                      BEFORE 2215, 88 MIN
                                      AFTER 2215, 47 MIN
                 O PLANT
                 • PLANT
            INFLUENT
            EFFLUENT
                           I
           2200
2300
TIME OF DAY
2400
0100
    FIGURE 24.  STORM EFFECT ON BOD AND COD - 9/16-17/71
                            -48-

-------
   500
   400
   300
   200
   100
            —I	1	1	
                     CONDITIONS

             REGENERATED  CARBON 6 500 mg/Z
             DETENTION  TIME: 88 MIN

                O  PLANT  INFLUENT
                •  PLANT  EFFLUENT
  2500
  2000
o-
E
  1500
  10UU
Q_
00
   500
        I
       0400
0500            0600
       TIME  OF  DAY
0700
          FIGURE  25.   STORM  EFFECT ON  TURBIDITY AND
                       SUSPENDED SOLIDS - 5/2/72
                              -49-

-------
O
O
CD
   300
   200
   100
  1000
   800
   600
   400
   200
    I        T       I

        CONDITIONS

REGENERATED CARBON 0  500 mg/X.
DETENTION TIME:  88 MIN

   O PLANT INFLUENT
   • PLANT EFFLUENT
        0400
                        _L
                      0500              0600
                              TIME  OF  DAY
                   '»	•—f
                  0700
      FIGURE  26.  STORM EFFECT  ON BOD AND COD  -  5/2/72
                               -50-

-------
                CONDITIONS
        REGENERATED  CARBON  0  500  mg/£
        DETENTION  TIME:   88 MIN
Q

CO
   300
   200
   100
o PLANT
0 PLANT
INFLUENT
EFFLUENT
   400
00
Q
O
00
Q
LjJ
Q
   300
   200
   100
              0200
                   0300
                   TIME OF DAY
                          0400
0500
            FIGURE 27.   STORM EFFECT ON TURBIDITY AND
                         SUSPENDED SOLIDS  -  5/16/72
                               -51-

-------
  600
  500
  400
=rf

en
  300
o
o
  200
   100
     CONDITIONS

REGENERATED CARBON
  @ 500 mg/£
DETENTION TIME:
  88 MIN
   o PLANT INFLUENT,
       TOTAL
   A PLANT INFLUENT,
       SOLUBLE
   • PLANT EFFLUENT,
       TOTAL
   120
 e   80
0
CO
    40
                                0	f	•—•—- •	f-
                                                            I
           0200
                   0300            0400
                     TIME OF  DAY
0500
        FIGURE 28.  STORM EFFECT ON COD AND  BOD - 5/16/72
                                -52-

-------
   800
                                      CONDITIONS
Z3  600
i—
•-3


>-

~  400
   200
                              REGENERATED CARBON  &  500
                              DETENTION TIME:   88 WIN

                                   PLANT INFLUENT
                                   PLANT EFFLUENT
  1600
O
CO
UJ

O
   1200
    800
   400
                          I
                                                         I
         0500
                        0600             0700
                            TIME  OF  DAY
0800
          FIGURE 29.  STORM EFFECT ON TURBIDITY AND
                      SUSPENDED SOLIDS  -  5/16/72
                             -53-

-------
1000  -
                                  CONDITIONS
                          REGENERATED  CARBON  0  500 mg/P.
                          DETENTION  TIME:  88  MIN
                             O PLANT  INFLUENT,  TOTAL
                             A PLANT  INFLUENT,  SOLUBLE
                             « PLANT  EFFLUENT,  TOTAL
       0500
0600            0700
    TIME OF DAY
030D
  FIGURE  30.   STORM EFFECT  ON  COD AND BOD -  5/16/72
                           -54-

-------
  6000
  5000 -
  4000 -
  3000 -
CD
ct:
  2000 -
  1000 _
  8000 -
  6000 -
oo
o
  4000 -
  2000 -
              CONDITIONS
REGENERATED  CARBON
    500 mg/K.
DETENTION TIME:
     MIN
            O PLANT INFLUENT
            • PLANT EFFLUENT
          2000
                2200            2400
                     TIME OF DAY
                                                         0200
         FIGURE 31.   STORM EFFECT ON TURBIDITY AND
                       SUSPENDED  SOLIDS  -  5/16-17/72
                             -55-

-------
inoo -
                                      CONDITIONS
                              REGENERATED CARBON  0  500  mg/J,
                              DETENTION TIME:  88  MIN
                                 O PLANT INFLUENT,  TOTAL
                                   PLANT INFLUENT,  SOLUBLE
                                   PLANT EFFLUENT,  TOTAL
        2000
2200            2400
    TIME  OF  DAY
                                                      0200
  FIGURE  32.   STORM EFFECT ON COD  AND BOD  -  5/16-17/72
                            -56-

-------
These observations are supported by a series of jar tests
which were run during the course of the 7/29/71 storm.  Four
samples collected during increasing, peak, decreasing and minimum
solids loading periods were examined with the results presented
in Figures 33 and 34.  The data in these figures emphasize
the important role of effective plant solids removal during a
storm.  The points corresponding to 0 carbon dose represent
the unfiltered supernatant liquid after alum and polyelectro-
lyte treatment.  A large portion of the total BOD and COD was
removed without the use of carbon; in fact, at peak solids
loading, over 90 percent of both BOD and COD were removed.
However, even at this level of removal, a residual COD of
92 mg/1 remained at the storm peak solids loading.  Thus, alum
coagulation alone is not sufficient to produce a low COD
effluent.  These jar test data suggest that as the storm
progressed and the COD was increasing, a carbon dose of 600
mg/1 was warranted to effect good COD removal.  Once the storm
peak was passed, however, the carbon dose could be reduced to
the 200-300 mg/1 level with virtually complete removal of all
sorbable COD.

During the course of each of the storms, the suspended solids,
COD, and BOD profiles of the wastewater followed the turbidity
profile with the peaks of the curves usually occurring at the
same time.  In some instances, the BOD and/or COD tended to
peak slightly ahead of the turbidity.  It was noted that the
soluble COD followed the same general pattern as the total
COD.  These observations suggest that turbidity can be used to
monitor trend variations in other influent parameters as a storm
progresses.  A decrease in turbidity should be indicative of
a corresponding decrease in soluble organics.  Therefore,
after the turbidity has peaked, it should be possible to
effect virtually complete removal of sorbable organics at a
substantially reduced carbon dose until the storm has sub-
sided at which time normal operation could be resumed.
Depending upon the effluent quality required and upon the
wastewater characteristics at a particular site, it would
be possible to operate the treatment process throughout storm
periods at a much lower carbon dose than the 600 mg/1 indi-
cated for raw sewage treatment.  Thus, operating economies
could be introduced by operating at a low carbon dose for
an entire storm period or by reducing the carbon dose after
the peak organic loading had occurred.  The second of these
alternatives assures the highest effluent quality at the
lowest cost.

Prior to the 9/13/71 and 9/16/71 storms, the New York State
Department of Environmental Conservation installed a flow-
meter in the sewer from which the plant influent was drawn.
Therefore, it was decided to attempt to adjust the pilot
plant flow rate to parallel the flow in the sewer during
                               -57-

-------
  120
  100 -
   80
   60
   40
   20
cr
E
Q
C
cc

OL
o

g 100
   80
   60
   40
   20
~l	1	1	

  SOLIDS  INCREASING
     1630  HOURS
    RAW SAMPLE

    COD 312  mg/£
    BOD  83  mg/£
    S.S.128  mg/£
             _L
   STORM PEAK
   1715  HOURS

   RAW SAMPLE

   COD 1216 mg/£
   BOD  375 mg/Jl
   S.S  446 mg/£
             200    400   600   800  1000   1200   1400   1600
                     FIXED CARBON DOSE  (mg/£)
        FIGURE 33.   JAR TEST DETERMINATION OF CARBON
                      REQUIREMENTS DURING INCREASING
                     AND PEAK LOADING  OF  7/29/71 STORM
                             -58-

-------
o
CO
o
o
    80
    60
    40
    20
   100
    80
    60
    40
    20
                    SOLIDS DECREASING
                       1745 HOURS
                       RAW SAMPLE
                       COD 752  mg/e,
                       BOD 188  mg/5
                       S. S.624  mq/X,
                     MINIMUM LOADING
                       2000 HOURS
                       RAld SAMPLE

                       COD 208 mg/5,
                       BOD  69 mg/£
                       S.S.352 mq/d
         0    200
400   600    800   1000   1200
  FIXED CARBON  DOSE  (mq/.O
                                                 1400
1600
  FIGURE 34.   JAR TEST  DETERMINATION OF CARBON REQUIRE-
                  MENTS  DURING DECREASING AND  MINIMUM
                       LOADING OF  7/29/71 STORM
                            -59-

-------
subsequent storms.  Attempts to accomplish this goal during
the 9/13/71 and 9/16/71 storms were not completely successful.
However, during the latter storm, the pilot plant flow rate,
initially at 35 gpm, was increased to 75 gpm in less than two
minutes during peak storm loading with no observable effluent
quality deterioration or operational upsets.  Thus, it appears
that plant performance is highly insensitive to rapid changes
in flow rate if chemical doses are rapidly adjusted to
correspond to the increased flow.

Pilot plant operations have demonstrated that it is possible
to produce a high quality product water from combined
sewage in a total treatment time of 50 minutes.  Moreover,
the system can accommodate rapid changes in flow and compo-
sition.  It appears feasible that a system based on this
process could be highly automated.  Carbon and chemical
doses could be controlled on the basis of flow and/or
turbidity monitoring to assure maximum system reliability
with minimum chemical usage.

MUNICIPAL SEWAGE TREATMENT

During most of the 1971 campaign, grab samples of the plant
influent and effluent were routinely collected at two hour
intervals and composited over a twenty-four hour period of
plant operation.  Several determinations of the diurnal
variations in influent and plant effluent quality were made
during this portion of the program.  Particular emphasis was
placed on this approach during the period when regenerated
carbon and reclaimed alum were in use.  Plant operational
data for the 1971 portion of the program are given in Tables
4 and 5 and the results are presented in Table 6 and in
Figures 35-47.

The diurnal data showed BOD and COD peaks in the plant
effluent which could not be explained by variations in
influent quality or by operational upsets.  These peaks are
evident in the curve presented in Figure 37.  Later runs in
which the influent waste stream was sampled on an hourly
basis, as in Figures 40, 42, 44, and 46, indicated rapid
fluctuation in influent quality.  High BOD and COD peaks of
perhaps an hour's duration frequently occurred.  These
inordinately high COD peaks (as great as 5200 mg/1) appeared
to occur on a fairly regular basis and were totally unexpected
in a predominantly residential area presumably free of
industrial wastes.

Observation of the highly variable nature of the influent
quality at the Albany site suggested that the two hour samples
composited over a twenty-four hour period migiht not be com-
pletely representative of the waste stream.  Reexamination of
                            -60-

-------
                TABLE  4
PLANT OPERATIONAL DATA FOR  1971  STUDIES
          USING VIRGIN CARBON


Date
6-7-71
8
9
10
14
15
16
17
21
28
7-21-71
13
14
15
16
19
21
22
26
2-7
8-11-71
25
26
30
9-1-71
2
9
Wastewater
Flowrate
(gpm)
40
40
40
40
40
40
40
40
40
40
40
40
40
72
72
70
70
73
69
70
41
43
45
72
64
62
70
Detention
Time
(min)
88
88
88
88
88
88
88
88
88
88
88
88
88
44
44
45
45
44
45
45
86
82
78
44
55
57
45
Polyelectrolyte Carbon
Dose
(mg/1)
6.0
6.0
4.0
4.0
2.0
2.0
2.0
2.0
2.0
2.0
2.0
2.0
2.0
2.2
2.0
2.0
1.5
1.7
1.2
2.0
3.5
2.6
2.7
2.8
2.5
2.7
2.9
Dose
(mg/1)
800
800
1000
1000
1000
1000
1000
800
400
800
1170
1330
1180
865
800
625
800
800
630
790
550
590
486
573
950
880
950
Carbon Type

Aqua Nuchar
Aqua Nuchar
Aqua Nuchar
Aqua Nuchar
Aqua Nuchar
Aqua Nuchar
Aqua Nuchar
Aqua Nuchar
Darco XPC
Darco XPC
Darco XPC
Darco XPC
Darco XPC
Darco XPC
Darco XPC
Darco XPC
Darco XPC
Darco XPC
Darco XPC
Darco XPC
Aqua Nuchar
Aqua Nuchar
Aqua Nuchar
Aqua Nuchar
Aqua Nuchar
Aqua Nuchar
Aqua Nuchar

-------
                 TABLE 5
PLANT OPERATIONAL DATA FOR DIURNAL STUDIES
Detention
Time
Date (min)
7/12-13/71
7/14-15/71
8/17-18/71
9/28-29/71
10/4-5/71
10/7-8/71
10/13-14/71
10/18-19/71
10/25-26/71
4/14-19/72
4/24-26/72
5/1-10/72
5/15/23/72
6/7-12/72
6/13-15/72
6/16/72
88
88
112
50
50
50
50
50
50
50
88
88
88
88
88
88
Carbon
Dose
(mg/1)
1170
1190
550
656
482
357
440
440
537
621
657
601
506
570
632
640
Lime
Dose
(mg/1)
__
--
119
165
220
178
248
194
171
237
140
165
213
226
203
182
Acid
Usage
(Ib/lbC)
__
--
0.32
0.64
0.91
0.57
0.66
0.43
0 .67
0.48
0.59
0.60
0.76
0.62
0.74
0.65
                                          Carbon Type

                                          Darco XPC
                                          Darco XPC

                                          Aqua Nuchar

                                          Regenerated

                                          Regenerated
                                          Regenerated
                                          Regenerated
                                          Aqua Nuchar
                                          Regenerated
                                          Aqua Nuchar
                                          Regenerated

                                          Regenerated
                                          Regenerated

                                          Regenerated
                                          Regenerated
                                          Regenerated

-------
                                           TABLE 6
                                plant Performance Data During
                              1971 Operations Using Virgin Carbon
CTl
Ul
1
  Date

6-7-71
  8
  9
 10
 14
 15
 16
 17
 21
 28

7-12-71
  13
  14
  15
  16
  19
  21
  22
  26
  27

8-11-71
  25
  26
  30

9-1-71
  2
  9

Note:
COD
Influent
400
238
442
365
280
270
355
228
448
114
340
265
220
258
399
254
96
346
119
268
195
235
233
269
210
217
242
(mg/1)
Effluent
35
28
46
28
52
50
40
34
68
20
36
35
30
40
25
12 -
12
31
24
20
55
45
19
38
45
27
50
BOD
Influent
113
90
96
--
--
89
99 ,
91
150
50
120
96
78
47
--
108
32
101
46
107
72
105
122
129
105
82
107
(mg/1)
Effluent
32
27
17
—
__
6
13
17
25
6
20
20
19
7
--
4
7
14
5
15
29
18
25
15
28
20
25
                                                                               SS  (mg/1)
                                                                         Influent  Effluent
192
62
73
135
86
92
102
108
152
128
206
73
72
70
94
416
102
63
106
43
106
98
78
104
78
9S
21
21
5
10
8
3
7
9
4
3
5
10
3
4
4
3
9
4
3
6
4
7
24
29
12
6
                    Samples  were  composited  over  24  hr  periods  from  grab  samples  at
                    2  hr  intervals

-------
                                  CONDITIONS
                          VIRGIN DARCO XPC @ 1170 mq/'J
                          DETENTION TIME:  88 MI
                                    O PLANT INFLUENT

                                    • PLANT EFFLUENT
0800
1200
1600
2000    2400
TIME OF DAY
0400
0800
      FIGURE  35.   PLANT SUSPENDED  SOLIDS AND
                   TURBIDITY REMOVAL 7/12-13/71
                        -64-

-------
               800
                                                  CONDITIONS

                                       VIRGIN DARCO XPC @ 1170
                                       DETENTION TIME:  88 MIN

                                              O PLANT INFLUENT
                                              • PLANT EFFLUENT
                                                                           mg/SL
               600  —
 i
CTl
(J\
cn
E
            O
            O
               400
               200  —
                            1200
                           1600
                      2000       2400

                   TIME OF  DAY

FIGURE 36.  PLANT COD REMOVAL 7/12-13/71
0400
0800

-------
                                  CONDITIONS
                          VIRGIN DARCO XPC @ 1190 mg/£
                          DETENTION TIME: 88 MI
                              O  PLANT INFLUENT

                              •  PLANT EFFLUENT
1000    1400
1800    2200    0200
        TIME OF DAY
0600
1000
       FIGURE 37.   PLANT SUSPENDED SOLIDS AND
                   TURBIDITY REMOVAL - 7/14-15/71
                         -66-

-------
           500
   400
                                  CONDITIONS

                       VIRGIN  DARCO  XPC  @  1190  mg/i
                       DETENTION  TIME: 88  MIN

                             OPLANT  INFLUENT
                             • PLANT  EFFLUENT
           300
 i
en
        en
        E
o
o
           100
           200  -
                        1600
                           2000
2400
0400
0800
1200
                                         TIME OF  DAY
                         FIGURE 38.  PLANT COD REMOVAL 7/14-15/71

-------
500
                                    CONDITIONS
                           VIRGIN AQUA NUCHAR @ 550 mg/
                           DETENTION TIME: 112 MIN
                                         PLANT  INFLUENT
                                         PLANT  EFFLUENT
      0800
1200
1600     2000     2400
     TIME  OF  DAY
                                             0400
                                       0800
   FIGURE 39.  PLANT COD AND BOD REMOVAL 8/17-18/71

                          -68-

-------
 1000
  800
  600
Ol
E
O

S 400
  200
  100
   80
   60
      CONDITIONS

ONCE REGENERATED CARBON
@ 656 mg/fc

DETENTION TIME:  50 MIN

          O PLANT INFLUENT
          • PLANT EFFLUENT
a
o
   40
   20
    0200    0600   1000     1400     1800
                            TIME  OF  DAY
           2200
0200  0400
      FIGURE 40.   PLANT COD AND BOD REMOVAL 9/28-29/71

                            -69-

-------
  350
  300 —
  250
=><

CD
CO
Q
O
CO
                                   1 - 1
                                  CONDITIONS
                       TWICE REGENERATED CARBON @ 482 mg/£
                       DETENTION TIME: 50 MIN
                                       OPLANT  INFLUENT
                                       ®PLANT  EFFLUENT
  200
  150
  100 —
          0400   0800
1200    1600    2000
  TIME OF DAY
2400   0400
    FIGURE 41.  PLANT SUSPENDED SOLIDS REMOVAL  10/4-5/71


                           -70-

-------
2500
            CONDITIONS
        TWICE  REGENERATED CARBON
        @  482  mg/£
        DETENTION TIME:  50 MI
        O PLANT INFLUENT
        • PLANT EFFLUENT
                                              2200   0200
  0200    0600     1000     1400     1800
                     TIME  OF  DAY
FIGURE 42.  PLANT COD AND BOD REMOVAL 10/4-5/71
                          -71-

-------
        200
                                                 CONDITIONS
                                           THREE TIMES REGENERATED
                                             CARBON @ 357 mg/i
                                           DETENTION TIME:  50 MIN

                                               O PLANT INFLUENT
                                               • PLANT EFFLUENT
NJ
I
     co
     Q
     Q
     LU
     O
     ^
     LU
     Q_
     I/O
TOO
                            I
                            I
                          0800             1600            2400           0803

                   FIGURE  43.   PLANT SUSPENDED SOLIDS REMOVAL 10/7-8/71

-------
               THREE TIMES REGENERATED  CARBON @ 357 rug/*.
               DETENTION TIME: 50 MI
                        OPLANT INFLUENT
                        •PLANT EFFLUENT
  1000    1400      1800    2200     0200    0600     1000

                       TIME OF DAY


FIGURE 44.   PLANT  COD AND  BOD REMOVAL  10/7-8/71

                        -73-

-------
     500
     400
         CONDITIONS
FOUR TIMES REGENERATED CARBON
  @ 440 mg/£
DETENTION TIME:  50 MIN

      OPLANT INFLUENT
      «PLANT EFFLUENT
 CFl
 E
O

—I
CD
LU
O
    300
    200
    100   -
                 0200
            FIGURE 45
           0600
1000
                                                 1400
                                          1800
                                                                     2200
                     TIME  OF  DAY
        PLANT SUSPENDED SOLIDS REMOVAL  10/13-14/71

-------
   2500
   2000
   1500
g  1000
    500
      CONDITIONS

FOUR TIMES REGENERATED
  CARBON @ 440 mg/£
DETENTION TIME:  50 MIN

    O PLANT INFLUENT
    • PLANT EFFLUENT
o
CO
    800  -
    600  —
    400  —
    200

    100
             2400
             0800          1600

              TIME OF DAY
2400
    FIGURE 46.  PLANT COD AND BOD REMOVAL 10/13-14/71

                          -75-

-------
   400
   300
   200
   100
               CONDITIONS

        ONCE REGENERATED CARBON
          @ 537 mg/£
        DETENTION TIME: 50  MIN
                 O PLANT  INFLUENT

                 • PLANT  EFFLUENT
en
E
O
CO
   400
    300
    200
    100
     0800
1600           2400

       TIME OF DAY
0800
   FIGURE 47.  PLANT COD AND BOD  REMOVAL  10/25-26/71

                         -76-

-------
the data compiled on the two hour sampling schedule indicated
that it was highly probable that the high COD peaks were
frequently missed in the influent samples.  On the other hand,
these peak loadings tended to spread out over a longer period
of time in the pilot plant and had an influence on effluent
quality for a 2 to 3 hour interval.  Therefore, they were
detected in the effluent samples.  Thus, the net result of
missing the high influent BOD and COD peaks should have been
to make the plant performance  (on a percent removal basis)
appear somewhat poorer than was actually the case.

Average plant effluent BOD, COD, and suspended solids concen-
trations for the 1971 studies were 17.8, 35, and 7.7 mg/1
respectively.  This represents removals of 02.3 percent BOD,
87.3 percent COD, and 94 percent suspended solids.

Prior to the start of the 1972 operations, an automatic
sampling system which continuously composited influent and
effluent samples for one or two hour sampling periods was
installed.  Data collected in this manner confirmed the
high variability of the sewage strength.  Although the COD
peaks observed in the 1971 data were much subdued due to
the averaging quality of the composite samples they were
nevertheless present.  Examination of the data shows that
the plant effluent quality significantly deteriorates
following these peak COD loadings.

Plant operational data for the 1972 studies are given in
Table 5 and performance data are presented in Figures 48-59.
In general, results were comparable to those observed in the
1971 portion of the program.  During the 1972 operations the
average effluent turbidity, suspended solids, COD, and BOD
concentrations were 0.67 JTU, 3.1 mg/1, 39 mg/1, and 17 mg/1,
respectively.  This represents average removals of 98.1 per-
cent suspended solids, 82.6 percent COD, and 81.3 percent
BOD.

Effluent quality frequency distribution curves for BOD, COD,
and suspended solids for the diurnal pilot plant operation in
Albany are given in Figure 60.  Figure 61 contains removal
probability curves based on the pilot plant data for these
same parameters.

Data from the pilot studies indicate that at times there was
a significant non-adsorbable organic component present in the
wastewater at the Albany site.  When present, this non-
adsorbable fraction represented BOD and COD residual of
10-20 mg/1 and 20-50 mg/1, respectively, which could not be
removed even at carbon doses as high as 1000 mg/1.

A significant non-adsorbable fraction was not detected in
the Richland, Washington studies with powdered carbon nor in
                          -77-

-------
C7-,
e
GO
O
o
I/O
o
   400
   300
   200
   100
            CONDITIONS

VIRGIN AQUA NUCHAR  @ 621 mg/X,
DETENTION TIME: 50 MIN

       O PLANT INFLUENT
       A PLANT EFFLUENT
   400   -
   300   -
   200   -
   100   -
               2400
             2400     1200

             TIME OF DAY
2400
                                                          1200
          FIGURE  48.   PLANT SUSPENDED SOLIDS AND
                       TURBIDITY  REMOVAL - 4/14  &
                                4/17-19/72
                              -78-

-------
                                     CONDITIONS
400
300
200
100
                           VIRGIN AQUA NUCHAR  @  621  mg/£
                           DETENTION TIME:  50  MIN
          4/14/72
          4/17-19/72-
                                    O PLANT  INFLUENT
                                    A PLANT  EFFLUENT
            2400
         FIGURE 49.
    2400     1200

     TIME OF DAY
2400
1200
PLANT COD AND  BOD REMOVAL
4/14 and 4/17-19/72
                           -79-

-------
                              T
en
E
o
C/1
UJ
O
IT
UJ
CL.
OO
    400
    300
    200
    100
              CONDITIONS

ONCE REGENERATED CARBON @  657 ma/!
DETENTION TIME: 88 MIN

          O PLANT INFLUENT
          A PLANT EFFLUENT
    150 I-
    100 I-
CO
o:
     50  \-
                 2400
           FIGURE  50.
           2400        1200

             TIME OF  DAY
                                                     2400
      PLANT SUSPENDED SOLIDS AND
      TURBIDITY  REMOVAL 4/24-26/72
                               -80-

-------
   600
   500
   400
     CONDITIONS
  ONCE REGENERATED
  CARBON @ 657 mg/H
  DETENTION TIME:
|_88 MIN
   O PLANT INFLUENT
   A PLANT EFFLUENT
 0}
 en
   300
   200
   100
  300
  200
en
E
O
§ 100
              1200        2400       1200        2400
                            TIME OF DAY
     FIGURE 51.   PLANT COD AND BOD REMOVAL 4/24-26/72
                            -81-

-------
              5/9-10/72
     CONDITIONS
TWO TIMES REGENERATED
CARBON 0 601 mg/i>
DETENTION TIME :  88 MIN
            OPLANT INFLUENT
           A PLANT EFFLUENT
2400      1200     2400     1200     2400
                  TIME OF DAY
   FIGURE 52.   PLANT SUSPENDED SOLIDS AND
                    TURBIDITY REMOVAL
                  5/1-3/72 & 5/9-10/72

                    -82-
                        1200

-------
     —i	1	r
              CONDITIONS
      TWO  TIMES  REGENERATED
      CARBON  @ 601  mg/SL
      DETENTION  TIME:  88  MIN
400
300
                                            T
                                  O PLANT  INFLUENT
                                  A PLANT  EFFLUENT-
2400     1200     2400      1200
                   TIME OF DAY
                                           2400
                                                     1200
        FIGURE 53.   PLANT COD AND BOD  REMOVAL
                     5/1-3/72 and 5/9-10/72
                          -83-

-------
         5/16-17/72
                              CONDITIONS
                         THREE TIMES
                         REGENERATED CARBON
                           506 mg/£
                         DETENTION TIME :  88 MI
                             O PLANT INFLUENT
                             APLANT EFFLUENT
               2400      1200
                 TIME OF DAY
FIGURE 54.
                         1200
PLANT TURBIDITY  AND SUSPENDED
       SOLIDS  REMOVAL
    5/16-17/72 & 5/23/72
                    -84-

-------
              i         r
              5/16-17/72-
                          1   9
                     -5/23/72-L
                         CONDITIONS
  600
  500
  400
  300
  200
  100
  200 -
   100 -
O
CO
THREE TIMES REGENERATED
CARBON @ 506 mg/£
DETENTION TIME:  88 MIN
        O PLANT  INFLUENT
          PLANT  EFFLUENT
             1200
        FIGURE 55.
   2400      1200
      TIME  OF  DAY
                                           1200
  PLANT  COD AND BOD REMOVAL
  5/16-17/72 and 5/23/72
                         -85-

-------
     300
     200
     100
                I       I     I    I      I
                        CONDITIONS
               FOUR TIMES REGENERATED CARBON
               @ 570 mg/£
               DETENTION TIME:  88  MIN
                   ORLANT INFLUENT
                   APLANT EFFLUENT
                                6/12/72-
     200 -
     150 -
     100 -
             2400
                     1200 2000  1200
                     TIME OF  DAY
                      2000
FIGURE 56
PLANT TURBIDITY AND SUSPENDED
         SOLIDS  REMOVAL
      6/7-8/72  & 6/12/72
                       -86-

-------
   800
   600
   400
   200
    -5-7-8-72-
                                  n       r
                                 «-6-12-72-
           CONDITIONS

FOUR TIMES REGENERATED CARBON
  @ 570 mg/£
DETENTION TIME:  88 MIN
01
E
CO
   200
   150
   TOO
    50
                            O PLANT INFLUENT

                            A PLANT EFFLUENT
             2400    1200  2000 1200

                      TIME OF DAY
                               2000
      FIGURE  57.   PLANT COD AND BOD REMOVAL
                   6/7-8/72 and  6/12/72
                        -87-

-------
en
E
1/1
Q
O
GO
Q
UJ
Q
   150
   TOO
    50
   150 -
   100 -
CD
Di
                CONDITIONS

FIVE TIMES REGENERATED CARBON @ 632 mg/£
DETENTION TIME:  88 MIN

            OPLANT INFLUENT          -

            A PLANT EFFLUENT
                         /L^
        1600     2400    0800   1600    2400

                             TIME OF DAY
                          0800
        FIGURE  58.   PLANT TURBIDITY AND SUSPENDED
                            SOLIDS REMOVAL
                              6/13-15/72
                            -88-

-------
  600
  500
  400
  300
o
O
  200
  100
             	1	1	

                   CONDITIONS

             FIVE TIMES
             REGENERATED CARBON
             @  632 mg/S,

             DETENTION  TIME:  88  MIN

                  O PLANT INFLUENT

                  A PLANT EFFLUENT
  150 -
Q
O
CO
  100 -
        1600   2400


          FIGURE 59.
 0800     1600    2400
     TIME  OF  DAY
0800
PLANT COD  AND BOD REMOVAL
6/13-15/72
                            -89-

-------
o
Q-

eC
I—

a

u_
o


o

UJ

0-
UJ
35

30


25


20


15


10


 5
 20


 15


 10


 5
1J1
                               SUSPENDED SOLIDS
                          12       16

                     EFFLUENT  SS
                                    20
24
                                       COD
                                        n
          25      50      75     100

                    EFFLUENT COD (mg/H\
                                   125
150
 20


 15


 10
                                        BOD
     10       20       30      40       50

               EFFLUENT  BOD  (mg/£)
                                                  60
       FIGURE  60.   FREQUENCY  DISTRIBUTION  OF  PILOT

                       PLANT  EFFLUENT QUALITY
                           -90-

-------
•X.
CO
o
        1 .0


        0.8


        0.6


        0.4


        0.2
                                       BOD
                                          I
               40   50   60   70  80   90   TOO

                          REMOVAL (•;)

FIGURE 61.  CUMULATIVE  PROBABILITY DISTRIBUTION  OF
             ACHIEVING REMOVAL  PERCENTAGES  GREATER
                 THAN OR EQUAL TO A GIVEN VALUE
                           -91-

-------
pilot studies with granular carbon by others(6'7'8), but was
observed in a recently completed pilot study in Cleveland,
Ohio (^'.  This suggests that in some cases, physical-chemical
treatment of raw municipal wastes may not achieve greater
than secondary levels of biodegradable organic removal while
in other instances, tertiary levels can be realized.  Each
waste stream must be examined on a case by case basis to
determine the level of BOD removal which can be achieved.
Although, for a significant portion of the time, tertiary
levels of BOD and COD removal were achieved at the Albany
site, on an average basis tertiary levels of BOD and COD
removal were not achieved.  Tertiary turbidity and suspended
solids effluent quality were consistently realized in the
pilot operations.

One of the attractive features of the powdered carbon treat-
ment process is the ability to vary the carbon dose with the
strength of the influent waste stream.  Although any attempt
at continuous variation in carbon dose would probably present
operational problems which would render this approach im-
practical, once a waste stream has been characterized, it
should be possible to operate at two or three predetermined
carbon doses during the course of a day.   In fact, this
concept was tested during the night hours at the Albany
site.  After it had been established that the influent
waste strength was fairly weak between the hours of 2200
and 0600, the carbon dose was reduced to 0-400 mg/1 during
this time period for several days with the results given
in Table 7.  These tests established that the carbon dose
could be drastically reduced during the nighttime hours
while maintaining a high quality effluent.  The data of
Table 7 indicate that suspended solids removal is independent
of carbon dose as would be expected.  Moreover,  in the 200
to 400 mg/1 range, BOD and COD removal is independent of
carbon dose during this portion of the day.  Subsequent to
these findings, during the months of September and October
1971, the carbon dose was routinely reduced to the 200 mg/1
level between the hours of 2200 and 0600 with no detectable
decrease in plant effluent quality.  Decreasing the carbon
dose to a low level during the portion of the day when the
wastewater has a low soluble organic content can signifi-
cantly reduce operating costs without sacrificing treatment
efficiency.  For example, if a plant v/ere operated at a
carbon dose of 600 mg/1 for sixteen hours a day and at 200
mg/1 for eight hours, the average carbon dose would be
substantially below 600 mg/1 (the actual dose would depend
upon flow variations).  Since carbon is the single most
important operating cost item in the treatment process, any
significant reduction in carbon dose represents a major
economy in operating costs.
                              -92-

-------
                   TABLE 7
PILOT PLANT PERFORMANCE AT LOW CARBON DOSES
      Plant Influent
Plant Effluent
Time
of Day
400 mg
2400
0200
0400
0600
200 mg
2400
0200
0400
0600
Suspended
Solids
(mg/1)
COD
(mg/1)
BOD
(mg/1)
Suspended
Solids
(mg/1)
COD
(mg/1)
BOD
(mg/1)
Carbon/1 8/19/71
33
14
18
21
162
116
58
37
58
37
21
29
5
7
7
5
17
21
12
12
9
10
6
3
Carbon/1 8/25/71
64
32
48
37
204
63
35
55
58
24
12
28
1
31
1
2
12
8
<1
4
8
3
2
3
0 Carbon 8/27/71
2400
0200
0400
0600
40
86
18
54
157
134
100
979
76
45
26
41
3
<2
4
4
54
23
37
54
19
12
8
14
                    -93-

-------
Although a high degree of soluble phosphorus removal was
achieved in the pilot operations, such a result is not ex-
pected in an operating plant.  In the pilot plant, excess
alum was added at times as discussed in Section VII of this
report.  However,  in actual plant operations, phosphorus
removed by the alum in early cycles would be recycled with
the regenerated carbon and recovered alum in later cycles.

An equilibrium condition would be established with no net
soluble phosphorus removal if there were no blowdown of
regenerated carbon.  However, since the phosphorus concen-
tration in the regenerated carbon-alum stream is high and
blowdown will be required, some phosphorus will be removed
from the system.  The makeup alum required by a five percent
blowdown will provide an anticipated equilibrium soluble
phosphorus removal of 31 percent.

The chlorine demand of the pilot plant effluent was investi-
gated.  Two samples drawn at different times of the day (1400
and 2200) were treated with various chlorine doses and allowed
contact times of 15 and 30 minutes as shown in Figure 62.  The
chlorine residual after 30 minutes contact averaged 0.2 mg/1
less than with 15 minutes contact.

Coliform analyses were run at various times of the day.  The
results in colonies/100 ml sample are presented below.
Time Sample Taken:             0600       0900      1600

Raw Sewage               1,150,000   4,700,000   15,900,000

Tube Settler Effluent '       872        18,000        7,500

Filter Effluent              584        14,100        7,000

Removal of coliforms in the plant was found to average 99.9
percent without disinfecting the effluent.   It was observed
that filtering the  tube settler effluent removed an additional
ten percent of the  clarifier effluent coliforms.

Filtration of the tube settler effluent at  the Albany site was
also observed to significantly improve pollutant removal per-
formance.  The filtered effluent averaged 7 percent lower"in
suspended solids and 20 percent lower in COD and BOD than the
tube settler effluent.  This may have been  due in large part
to the previously discussed operational problems associated
with the pilot tube settler.

The average neutralization lime usage was 190 mg/1.  As seen
from Figure 63, the dose varied substantially from run to run
                                -94-

-------
A  SAMPLED  1400  6-12-72  15 MIN CONTACT
A  SAMPLED  1400  6-12-72  30 MIN CONTACT
O  SAMPLED  2200  6-13-72  15 MIN CONTACT
•  SAMPLED  2200  6-13-72  30 MIN CONTACT
   FIGURE 62
              4                   6
      CHLORINE APPLIED (mg/v }

CHLORINE DEMAND OF PLANT EFFLUENT

-------
I
CTl
           "ul
           200
              o
           150
         CD
         
-------
such that no significant trend is observed.  It is anticipated
that a reduction in lime dose below this level can be achieved
since, as discussed in Section VII of this report, it is believed
that the acid requirement for alum recovery can be substantially
reduced below that employed in the pilot studies.

Discounting equipment failures in the pilot system, the treat-
ment process proved to be highly reliable and was capable of
consistently producing a high quality effluent.

REGENERATED CARBON PERFORMANCE

Regenerated carbon and reclaimed alum performed as well as the
virgin substances in the pilot system.  In all of the runs with
the recovered products, coagulation and sedimentation proceeded
normally.  The removal of organic matter from the raw waste-
water was good during the runs with regenerated carbon.  Data
on the system performance with virgin carbon and with regener-
ated carbon are presented in Table 8 and Figures 40-47 and
50-59.  It is evident from the data of Table 8 that even with
regenerated carbon at fixed carbon doses as low as 370 mg/1,
the pilot plant COD, BOD, and SS removals are comparable to
a virgin carbon dose of 600 mg/1.  After seven regeneration
cycles, the sorption performance of the carbon was essentially
that of virgin carbon as evidenced by the pilot plant data
and the jar test data presented in Figures 66-74  (Section VII).
                              -97-

-------
                                                   TABLE 8
                                  Regenerated Carbon Performance Comparison
                                       Plant Influent
                                                                  Plant Effluent
                                                                                         Plant Removal
Fixed
Carbon
Carbon Dose
Batch (mg/1)
Virgin*
1.0 Regenerations A
1.9 A
2.8 A
3.7 A
1
UD
CD
1




0.9
Virgin
1.0
1.9
2.9
3.8
4.8
B
C
C
C
C
C
C
600
650
580
370
470
540
601
633
570
506
570
632
COD BOD
(mg/1) (mg/1)
276 104
278
411
690
337 160
246
187
323
286
192
291
224
142
69
133
106
80
106
99
SS Turbidity COD
(mg/1) (JTU) (mg/1)
130
135
248
85
--
139
190
206
214
139
133
—
—
101
90
102
294
119
70
35
27
56
45
44
43
29
47
46
41
56
31
BOD SS Turbidity COD
(rag/1) (mg/1) (mg/1) %
17.8 7.
14 3.
23 7.
36 18.
14 3.
27
12
24
18
17
26
13
—
2,
2,
4,
4,
3,
3
.7 -
.7 -
.0 -
,2 -
.1 -
- -
.5 0
.5 0
.4 0
.2 0
.1 0
.9
_
-
.55
.84
.99
.66
.47
—
87
90
86
94
87
82
85
85
84
78
81
86
BOD
%
83
91
81
82
82
83
79
75
87
SS Turbidity
% %
94
95
93
96
—
98
99
98
98
98
97
—
—
>99
>99
99
>99
>99
—
*Data from two months operation, daily composite samples

-------
                          SECTION VII


                          REGENERATION


OPERATIONAL PROCEDURES

During that portion of  the  1971 pilot  studies that the carbon
regeneration  facility was operational, the  liquid treatment
system and carbon  regeneration system  were  operated alter-
nately on a campaign basis.  The treatment  system was
operated for  a  twenty-four  hour period or until approximately
500 pounds of activated carbon was consumed.  Sludge was
stored until  the treatment  operation was completed and then
was dewatered in the centrifuge and fed into the fluidized
bed furnace.

In the 1972 portion of  the  program, the liquid treatment
system and the  carbon regeneration system were operated
simultaneously.  For any given cycle,  the treatment portion
of the pilot  plant was  operated alone  until sufficient carbon
had been accumulated for the regeneration operation to
commence.  Both systems were then operated  until approximately
1000 pounds of  carbon was exhausted in the  treatment process.
The treatment system was then shut down until the next cycle
was begun.

Regenerated carbon-aluminum oxide slurry from the off gas
scrubber was  collected  in holding tanks during furnace
operation.  Supernatant water from these storage tanks was
continuously  decanted and recycled through  the venturi
scrubber until  the slurry concentration in  the tanks built
up to approximately six percent carbon, which was suitable
for use in the  treatment operations.   Cooling of the recycled
slurry from the venturi scrubber was not necessary since it
left the disengaging vessel at 60°C.   When  the slurry con-
centration in the  carbon tanks had reached  the desired
concentration,  a pH adjustment to pH 2 was  then effected with
sulfuric acid and  the necessary makeup carbon and alum were
added to the  storage tanks.

Samples of virgin  and regenerated carbon slurries were
-analyzed for  fixed carbon content.  Analyses were obtained by
combusting a  sample at  1200°C in a pure oxygen atmosphere
and then chromatographically determining the carbon dioxide
produced.  Reproducibility  using this  technique was con-
sistently within five percent.  Attempts were made to
analyze the fixed  carbon content of spent carbon sludge by
heating at selected temperatures to drive off organics prior
                                -99-

-------
to combusting a sample.  However, no reproducible results
could be obtained.  Since the fixed carbon content of the
sludge feed to the regeneration furnace could not be de-
termined, it was necessary to determine carbon los~^s on
the basis of a mass balance across the entire system.  Virgin
and regenerated carbons did not contain the organic component
which created analytical errors in carbon analysis of carbon
sludge samples.

Alum recovery was also determined on a mass balance basis.
Samples were drawn from each of the acidified carbon slurry
tanks, filtered through 0.45 micron membrane filter and the
filtrate was then analyzed for aluminum as outlined in
Standard Methods(10).

Due to the fact that the regeneration furnace became opera-
tional so late in the  1971 portion of the program, there was
only a limited time available for regeneration studies.  Thus
it was deemed necessary to complete each regeneration-reuse
cycle in the minimum time possible in order to achieve a
maximum number of cycles.  Therefore, there was insufficient
time to obtain analytical results on carbon recovery follow-
ing a regeneration cycle prior to commencing the next treat-
ment cycle of the operation.  As a result, 1971 carbon doses
in the treatment system were lower at times than desired.

Makeup activated carbon was not added in the first two 1971
regeneration cycles but was added routinely after the second
cycle in order to maintain a total quantity of 500 pounds of
fixed carbon.  Sufficient alum was added after each regenera-
tion to maintain the aluminum concentration in the feed
solution at 1.6 g/1.

In the 1972 operation, the carbon inventory was initially
maintained at 1000 pounds of fixed carbon.  Following the
fourth regeneration cycle, the inventory was reduced to 500
Ibs to decrease the time required per regeneration cycle.
Virgin carbon and alum were added as necessary to compensate
for losses.

At times it became necessary to begin using a tankful of
regenerated carbon before the results of the aluminum analysis
became available.   To  be certain of a minimum feed strength
of 1.6 g/1 aluminum,  alum was added beyond what was actually
required.  Thus the actual alum concentration in the treatment
system was sometimes higher than 200 mg/1.

SYSTEM STARTUP

Numerous mechanical problems with the furnace equipment were
encountered during the startup phase of the operation.  Most of
                          -100-

-------
these problems were minor in nature and were easily corrected.
However, several major difficulties of a more persistent nature
caused a significant delay in actual furnace operations.  These
major problems involved heat leakage around the hearth, lower
door, and burner.  A great deal of time and effort was expended
in resolution of these problems.  Final sealing of these leaks
involved replacement of the burner assembly and redesign and
replacement of the hearth and lower door.  Although the initial
construction of the furnace was complete on May 27, 1971, the
regeneration system did not become fully operational until
September 17, 1971.

During the 1971 operation, the extra strength castable hearth
developed deep cracks necessitating replacement twice during
the campaign.  This was corrected prior to commencement of
the 1972 operation by replacing the castable hearth with a
brick hearth and by modifying the controls such that the
combustion air system was automatically shut down in the
event of a flame failure.  Previously, following flame
failure, the combustion air at 150°F continued to blow into
the 1900°F firebox, thus not allowing the fluidized bed sand
to percolate through the hearth.  It is believed that the
thermal shock thus produced played a major role in previous
hearth failures.  Following these modifications, no major
startup problems were encountered in the spring of 1972.

FURNACE OPERATIONS

Due to the fact that the fluidized bed furnace became
operational so late in the 1971 portion of the pilot program,
there was little latitude for experimentation with the
operating conditions.  Using a ten inch diameter furnace, it
had previously been established that good carbon regeneration
and recovery could be obtained at a bed temperature of 1250°F
and an oxygen level of less than one percent in the stack
gas(11'12;.  Therefore, these conditions were followed in the
pilot runs at Albany.  Operating conditions for the fluidized
bed furnace are given in Table 9.  Bed velocities reported in
Table 9 are calculated at a point midway up the bed using the
superficial area at that point.  The gas velocity in the
freeboard zone is 0.785 times the reported bed velocity.

A total of six carbon regenerations were accomplished in
the pilot operations in 1971.  Runs 1-4 represent a single
batch (Batch A) of powdered carbon followed through consecu-
tive cycles of use and regeneration.  At the end of the fourth
regeneration, a substantial quantity of the carbon was lost
due to an operational problem; therefore, it was necessary
to begin again with virgin carbon at this point.  Runs 5 and 6
represent the first and second regenerations of the second
batch (Batch B) of carbon.  Runs 7-13 represent a single batch
(Batch C) of carbon regenerated seven times.
                          -101-

-------
                                                          TABLE 9
                                         FLUIDIZED BED-FURNACE OPERATING CONDITIONS
Regeneration No.
                                                                                         10
                                                                                                 11
                                                                                                        12
Solids Concentration in Feed (%)  21.7  24.1  22.9  22.6  23.5  22.9  22.0   21.1   21.9   21.9    23.5    25.7
                                                                                                                13


1
I—1
0
to
1



Carbon Batch
Bed Temperature (°F)
Firebox Temperature (°F)
Bed Velocity (ft/sec)

Recycle Gas Flow (SCFM)
Combustion Air Flow (SCFM)
Propane Flow (SCFM)
Sludge Feed Rate (Ibs/hr)
A
1290
1900
1.4

83
71
3.0
120
A
1260
1880
1.6

89
89
3.7
125
A
1250
1910
1.6

83
86
3.6
120
A
1250
2030
1.4

60
82
3.4
120
B
1250
1980
1.3

60
68
2.8
115
B
1260
1905
1.1

63
63
2.6
80
C
1280
1840
1.7

61
80
3.5
119
C
1270
1900
1.5

62
68
3.0
105
C
1260
1860
1.7

78
66
2.9
96
C
1250
1860
1.9

107
64
3.1
64
C
1260
1860
2.1

123
59
3.3
94
C
1240
1860
2.2

126
67
3.7
106
C
1220
1880
2.2

138
60
3.6
117

-------
Since it was impractical to completely drain all of the
carbon from the treatment system prior to each regeneration
cycle, a fraction of the carbon was not regenerated each cycle.
In the case of the 1971 runs, this represented 4-10 percent
of the carbon per cycle.  The result was that even though four
cycles were completed in the case of the first batch of carbon,
the actual number of regenerations was only 3.7.

Due to the larger carbon inventory of the 1972 runs, the
system holdup represented a smaller fraction of the total
carbon.  Runs 7-13, a total of seven cycles, provided 6.7
actual carbon regenerations.

The temperature of the fluidized sand bed was monitored by
four thermocouples evenly spaced around the bed at various
levels.  It was observed that temperatures at all four points
could be maintained within a 50°F range when the bed was
properly fluidized.  At low gas flow rates through the bed,
the thermocouple opposite the carbon feed point indicated
temperatures higher than the thermocouple adjacent to the
entering slurry.- a result of poor bed fluidization.  Tem-
peratures in the freeboard zone measured near the furnace
gas outlet consistently registered 50-100°F lower than the bed
temperature.

The firebox temperature was maintained below 2100°F to avoid
damage to the furnace material.  Temperature was regulated by
controlling the ratio of combustion air to recycle gas.  Re-
cycle gas entering at 150-200°F cooled the firebox while
keeping the oxygen level low and providing the proper
fluidization gas flow.

An effort was made to maintain the bed velocity at as low a
level as possible in order to minimize attrition of the sand
and also to prevent sand carryover with the carbon.  However,
it was observed that at fluidizing velocities of about 1
ft/sec or less, heat transfer from firebox to bed was much
poorer than at higher velocities.  During Run 3, at a velocity
of 1.6 ft/sec, 120 Ibs/hr of sludge could be fed while keeping
the bed at 1250°F and the firebox about 1900°F.  However,
when the fluidizing velocity was decreased, it was necessary
to substantially decrease the sludge feed rate to the furnace
in order to maintain the desired temperature.  For example,
in Run 6, when the fluidizing velocity was decreased to
1.1 ft/sec, the sludge feed rate had to be correspondingly
reduced to 80 Ibs/hr in order to maintain a bed temperature
of 1260°F.

It was necessary to maintain the combustion air blower in
continuous operation even when the regeneration furnace was
not in use in order to prevent the sand from flowing through
the holes in the hearth and into the firebox.  This contributed
                          -103-

-------
to attrition of the sand in the furnace which was observed to
be substantial.  Sieve analyses of the sand both before use
and after 21, 35, and 41 days of fluidization in the furnace
are presented in Table 10.  If attrition cannot be substantially
reduced, periodic withdrawal and replacement of the sand appears
indicated.  It is suggested that provisions for keeping the
sand above the hearth during blower shutdown be included in the
design of the hearth.  Proper installation of bubble caps may
provide good horizontal distribution of the gas while checking
sand flow into the firebox during blower shutdown.

The oxygen content of the fluidized bed off gas was determined
by Orsat Analysis.  Once the proper 02 level was attained, a
Hayes Model 635 oxygen analyzer continuously monitored the
level.  Periodic adjustments of the fuel-air ratio were made
as necessary to maintain the oxygen content of the stack gas
at the 0-0.5 percent level.

One of the major operational problems which occurred during
the course of the program was plugging of the holes in the
hearth.  Toward the end of the 1971 operations in Albany, the
pressure drop across the hearth rather suddenly increased to
the point where shutdown was necessary.  Inspection of the
system revealed that sand was caking inside the holes in the
hearth, thus  restricting the gas flow.

Prior to beginning the 1972 operation, a 6 inch layer of
3/4 inch diameter high temperature gravel was placed on top
of the hearth.  It was felt that this would provide an addi-
tional buffer layer between the 1250°F bed and the 2000°F
firebox as well as reduce the amount of sand that percolates
through the hearth during furnace shutdowns.  About two
weeks after regeneration began during the 1972 campaign, the
hearth pressure drop again became excessive.  Inspection of
the hearth revealed that the 6 inch layer of gravel on the
hearth had become cemented together into one large mass.
X-ray analysis showed the "cement" to contain a large amount
of magnetite.  (The presence of a mixture of FeO and Fe203 is
understandable since maintaining an oxygen level in the
fluidized bed slightly above zero required frequent adjust-
ments in operating conditions.  Although the furnace atmos-
phere was normally slightly oxidizing, at times, reducing
conditions probably existed.)  The caked sand removed from
the inside of the hearth holes also was found to contain
large amounts of magnetite.  Plugging of the holes in the
hearth continued to be a problem throughout the 1972 portion
of the program.

In addition to causing periodic system shutdown, plugging
presents other potential problems.  It is believed that as some
of the holes plugged with sand and magnetite, nonuniform
fluidization occurred.  In this case, spouting of the bed
                          -104-

-------
                          TABLE 10

             SIEVE ANALYSES OF FLUIDIZED BED SAND
                                                   Fraction
                                                   Quantity
                                                   Retained
                                                      1.67
                                                     63.04
                                                     31.81
                                                      3.10
                                                      0.37
                                                     99.99
                                                      0.38
                                                     41.97
                                                     49.28
                                                      5.41
                                                      1.55
                                                      0.37
                                                      0.67
                                                      0.36
                                                     99.99
                                                      0.21
                                                     28.78
                                                     33.07
                                                     14.97
                                                     10.68
                                                      5.83
                                                      6.23
                                                      0.23
                                                    100.00
                                                      0.56
                                                     26.58
                                                     33.09
                                                     18.24
                                                      9.90
                                                      5.49
                                                      4.90
                                                      1.23
Contained about 1 g of chunks of fused material from the furnace.
Sand Retained
on Screen #
Virgin Ottawa
20
30
40
50
Pan
Furnace Sand
20
30
40
50
60
70
100
Pan
Furnace Sand
20
30
40
50
60
70
100
Pan
Furnace Sand
20
30
40
50
60
70
100
Pan
Quantity
Retained
(g)
Flint Shot Sand
8.6
325.0
164.0
16.0
1.9
Collected After 21 Days Fluidization
0.89
99.18
116.46
12.79
3.66
0.88
1.59
0.86
236.31
Collected After 35 Days Fluidization
0.88
121.68
139.83
63.31
45.14
24.67
26.33
0.97
422.81
Collected After 41 Days Fluidization
2.4l
112.8
140.4
77.4
42.0
23.3
20.8
5.2
424.3
                              -105-

-------
material could occur causing increased sand carryover into the
product.  Uneven fluidization would also result in nonuniform
carbon retention times thus reducing the carbon regeneration
efficiency.

Identification of the source of iron became of major importance
since iron appeared to be the cause of the biggest operational
problem in the regeneration system.  An iron inventory for each
regeneration cycle was determined with the results as shown
in Figure 64.

It was noted that the actual iron inventory increased initially
and then leveled off at about 13 pounds.  However, when
physical losses were taken into account, the iron inventory
increased more or less constantly for the first five cycles at
about six pounds per cycle.  An identification of the possible
sources could  not account for anywhere near this quantity of
iron.  The maximum possible contributions of iron from various
sources were identified as follows

     Fe from sewage treated        0.39 Ibs per cycle
     Fe from lime impurities       0.35
     Fe from alum impurities       0.64
     Fe from H2SO4 impurities      0.01
     Total Fe                      1.39 Ibs per cycle

Thus a maximum of 1.4 pounds of iron per cycle could be
identified as possibly entering the system from known
sources.  This left 4.6 pounds of iron per cycle which could
not be attributed readily to any source.

When the holes in the hearth plugged, the caked material filled
the entire six inch length of the holes.  This suggested that
the iron was entering the system below the hearth since it
appeared unlikely that material could work down from the top
of the hearth and plug the holes in depth while the high
velocity gas stream was blowing upward through the holes.  In
addition, the absence of any significant quantity of aluminum
in the materials which caked in the hearth holes indicated
that a special source of iron introduced below the hearth was
responsible for the plugging.  Neither the fresh air stream
nor the propane stream were probable sources of large quanti-
ties of iron.  Therefore, it was deduced that the iron was
probably entering the firebox in the recycle gas stream.

Shortly after the iron buildup was discovered, the recycle
gas blower failed.  It was discovered that two of the
thirteen blower fans were severely corroded and consequently
were out of balance thus causing the blower failure.  Further
inspection of the remainder of the recycle gas system revealed
                          -106-

-------
]
)-•
o

1
                  30
                  20
     I          I


OACTUAL Fe INVENTORY


A Fe INVENTORY CORRECTED

  FOR PHYSICAL LOSSES
                                         }         9         10



                                         REGENERATION NUMBER
                                                       12
                     FIGURE 64.  IRON INVENTORY  IN REGENERATED CARBON  SLURRY

-------
that the inside of the six inch diameter black iron piping
was covered with a rust scale that was easily dislodged.
Following repair of the blower, the recycle gas stream was
closely observed and it was noted that large clouds of red
dust (presumably rust) were often present in the recycle
system at blower startup.  Thus, it was concluded that the
major source of iron which caused plugging of the hearth
derived from corrosion of the recycle gas system.

Design of a corrosion resistant recycle gas system should
eliminate the introduction of iron into the firebox and thus
should eliminate the hearth plugging problem.  This would
reduce the total iron buildup to a maximum of 1.4 pounds per
cycle or 0.0018 pounds of iron per pound of carbon used.
However, this residual iron should not cause plugging problems
in the hearth since it would be introduced into the fluidized
bed zone of the furnace and thus should not work down to plug
the hearth.  Installation of bubble caps should provide addi-
tional insurance against the hearth plugging from the top
down.  Therefore, it is concluded that the serious plugging
problems encountered in the Albany pilot plant operations
can be easily precluded by proper use of corrosion resistant
materials of construction.

The buildup of inert material in the carbon following each
regeneration is plotted in Figure 65.  Batch A regenera-
tions are characterized by a high initial increase in inert
material in the first regeneration cycle and then a gradual
increase in inert content at the average rate of 3.2 percent
per cycle for successive regenerations.  In the case of
carbon Batch B, insufficient data are available to establish
a trend.  Inert material buildup in the third batch of
carbon  (Batch C) followed the same general trend as that
established for the first carbon batch -- a high initial
buildup of inert material in the first regeneration cycle
and then a gradual increase in subsequent cycles, in this
instance at the rate of 2.8 percent per cycle.  During the
seventh regeneration cycle, the sand trap on the product
line failed for a portion of the run thus permitting a
higher than usual sand carryover into the product and conse-
quently, a higher inert buildup.

Average inert material buildup in the carbon for cycles
subsequent to the first cycle was 2.9 percent per cycle
for the entire pilot plant operation.  The average fixed
suspended matter of 23 daily composite sewage samples was
41 mg/1.  Considering that 94 percent of the suspended solids
are removed in treatment at a carbon dose of 600 mg/1, the
regenerated carbon should build up ash at the rate of 6.4
percent per cycle.  Actual pilot plant data show a 2.9 percent
buildup.  It is likely that acidification of the regenerated
carbon to pH 2 dissolves a significant quantity of the ash.
                          -108-

-------
1
H>
O

 1
            O

            CD
                         FIGURE 65.
2345


 NUMBER OF REGENERATION CYCLES


INERTS BUILDUP IN REGENERATED  CARBON

-------
Most of this dissolved ash is probably discharged in the
product water from the liquid waste treatment system.

Microprobe analyses of the inert material for cations of
molecular weight greater than Na revealed Si to be the over-
whelmingly predominant species.  This result was confirmed
by X-ray analyses which indicated Si02 was the main constituent
of the inert material.  These observations suggest that the
major component of the inert material in the product from the
regeneration furnace was sand.

Since the inert material in the regeneration carbon stream
built up at a regular rate for all but the first cycle, it is
apparent that special circumstances unique to the first cycle
in the cases of carbon Batches A and C must have been respon-
sible for the high initial jump in inerts.  Considering carbon
Batch A, the 15.5 percent increase in inerts in the first
regeneration cycle represents 122 pounds of material.  In the
case of carbon Batch C, 308 pounds of inert material were
required to cause the 30 percent jump in the first cycle.

It appears that a major portion of the inert buildup during
the first regeneration of carbon Batch C resulted as a conse-
quence of improper positioning of the plant influent hose in
the sewer.  Plant influent was drawn from a flat bottom area of
the sewer 7.5 feet wide used as a metering chamber.  The rear
edge of a 12 inch wide by 12 inch deep trench extending across
the chamber formed a weir with the depth of overflow being used
to determine flowrate.  The pilot plant influent line was
wedged into this trench to prevent its becoming dislodged dur-
ing high flows in the sewer.   The trench, however, contained a
large quantity of sediment and gravel which was drawn into
the pilot plant during the first few hours of operation.  In
fact, the vertical influent hose soon became plugged with
gravel.

During the 1971 operations the liquid treatment portion of
the plant was operated for several months before the regen-
eration facility became operational,  allowing ample time to
clear the sand and gravel from the trough •   On the other
hand, during the 1972 operation,  sludge was collected and
regenerated from the start of the treatment operations.  Thus,
the material sucked from the trough was fed to the furnace
with the sludge where it could be abraded and/or thermally
cracked in the fluidized bed and then find its way into the
product carbon stream.

It is believed that the major portion of the 308 pounds of
inert material buildup in the first regeneration of carbon
Batch C resulted from this cause.   Since a full scale plant
would have a grit chamber,  a problem of this nature should
not occur.  In fact,  a grit chamber should effect some
                          -110-

-------
reduction in inert material buildup in each regeneration
cycle and therefore, one would expect a lower average buildup
than observed in the pilot runs.

No sufficient reason for the high initial buildup of inert
material in the first regeneration cycle of carbon Batch A is
evident.  The cause cannot be attributed to a high initial
attrition of virgin sand and carryover in the product since
the furnace sand was completely replaced several times during
the pilot program and no high increase in inerts was evident
in subsequent regenerations.  Thus it appears that the source
of the inert material buildup in the first cycle regenerations
of both carbon Batches A and C was external to the regeneration
system and most probably consisted of material present in the
influent.waste stream.  A grit chamber should eliminate this
contribution of inerts to the regenerated carbon.

Following each regeneration cycle, jar tests were run with
samples of the regenerated carbon, duplicating as nearly as
possible the pilot plant operating conditions.  Data from
these jar tests are presented in Figures  66-74.  Examination
of this data indicates that the regenerated and virgin carbons
were virtually identical in sorptive capacity.  During the
first part of the first regeneration run (Batch A), highly
unstable temperature and sludge feed conditions persisted in
the regeneration furnace.  Figure 66 illustrates the adverse
effect that these unstable conditions had on recovery of the
sorptive capacity of the carbon.  Later in the run when the
system had stabilized, regeneration was much better as indi-
cated by the sorption curve in Figure 66.  The pilot plant
data for the regenerated carbon given in Table 8 substantiate
the observation that full capacity recovery could be achieved
after numerous regenerations.

ALUM RECOVERY

It is well known that aluminum hydroxide goes through the
conversion
     A1(OH)350°:C  Y-A1203            23

The Y-oxide readily dissolves  in sulfuric acid to yield
aluminum ions while the a-oxide is highly acid resistant.
Since carbon regeneration  is effected in the fluidized bed
furnace below 1000°C, the majority of the hydrous aluminum
oxide present in the carbon sludge should be converted to
the soluble alumina, i-Al2Ql'  in the regeneration process.  _The
laboratory  studies described  in Appendix A indicated that  it
should be possible to recover  80-100 percent of the aluminum
following regeneration.
                          -Ill-

-------
to
I
              160
               40  -
                                                O  VIRGIN  NUCHAR

                                                A  FIRST  1/3  OF  RUN

                                                D  LATTER  2/3 OF  RUN


                                                     RAW  SEWAGE  COD  436 mg/£
                              200          400           600


                                      FIXED  CARBON DOSE (mg/£/
800
                  FIGURE  66.   JAR TESTS ON ONCE REGENERATED CARBON  -  BATCH  A

-------
               200
OJ
1
            Q
            a
            o
            GO
            UJ
            Di
               100
                                                 O  VIRGIN

                                                 •  TWICE  REGENERATED CARBON
                                                         I
                                                                     _L
                                                                            I
                        TOO   200    300   »  400    500    600    700

                                       FIXED CARBON  DOSE (mg/£)
800   900
                   FIGURE 67.  JAR TESTS ON TWICE REGENERATED CARBON  -  BATCH A

-------
en
O
   120
   100
    80
    60
    40
    20
O VIRGIN CARBON

• THREE TIMES REGENERATED CARBON


     RAW SEWAGE COD 595 mg/£
                    I
                   200          400           600

                           FIXED  CARBON  DOSE (mg/O
                                           800
     FIGURE 68.   JAR TESTS ON THREE TIMES REGENERATED CARBON  - BATCH A

-------
en
1
              140
              120
              100
               80
               60
               40
    I       I      I      I


O VIRGIN CARBON

• FOUR TIMES REGENERATED CARBON


     RAW SEWAGE COD 357 mg/£
                                                                    I
                       200   400   600    800  1000   1200  1400  1600


                                     FIXED CARBON DOSE (mg/£)
                FIGURE 69.  JAR TESTS ON FOUR TIMES REGENERATED CARBON - BATCH A

-------
   140
                                O VIRGIN CARBON
                                A ONCE REGENERATED CARBON
                                D TWICE REGENERATED CARBON

                                     RAW SEWAGE COD 375 mg/£
                  200         400          600
                          FIXED CARBON DOSE  (mg/2/
800
FIGURE 70.  JAR TESTS ON ONCE AND  TWICE REGENERATED CARBON - BATCH C

-------
o!

CD
a
O
O
*—<
t/1
                              O  VIRGIN  CARBON

                              A  THREE  TIMES REGENERATED CARBON
                                    RAW SEWAGE COD 424 mg/£
    30  -
    20  -
    10  -
                   200          400          600

                           FIXED CARBON DOSE (mg/Jl)
800
    FIGURE 71.  JAR, TESTS  ON  THREE TIMES REGENERATED CARBON r BATCH C

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CO
I
              120
              100 —
            <=•;

            CD
           a
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           oo
O VIRGIN  CARBON

A FOUR TIMES  REGENERATED
                                                   RAW SEWAGE COD 353 mg/£
               20 _
                            200           400          600

                                      FIXED  CARBON DOSE (mg/£)
                       800
               FIGURE  72.   JAR TESTS ON FOUR TIMES REGENERATED CARBON  - BATCH C

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i
i-1
                                                       T
      T
                                               0  VIRGIN  CARBON
                                               A  FIVE  TIMES  REGENERATED
                                               0  SIX TIMES  REGENERATED
                                                     RAW  SEWAGE  COD  323 mg/£
I
                                           I
I
I
                       200   400   600   800    1000    1200   1400
                                      FIXED CARBON  DOSE  (mg/O
            FIGURE  73.   JAR TESTS  ON FIVE  AND SIX TIMES REGENERATED CARBON - BATCH C

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           50
                                                        OVIRGTN  CARBON
                                                        A SEVEN TIMES  REGENERATED  CARBON
                                                             RAW  SEWAGE  COD  53.5
o
I
       Q
       O
       Q

       t/1
       l_Lj
       cc.
           40
30
           20  —
           10  -
                            200
                                                                 800
                             400            600

                          FIXED CARBON DOSE (mg/JL)

FIGURE 74,   JAR TESTS ON SEVEN TIMES REGENERATED  CARBON - BATCH C

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In the pilot operations, alumina was conveyed from the furnace
with the carbon and deposited in the storage tanks.  Following
the carbon regeneration operation, the carbon slurry was
acidified to pH 2 with sulfuric acid in order to dissolve the
alumina and free aluminum ion.  The average recovery of
aluminum was determined to be 91.3 percent per regeneration
cycle in the 1972 pilot runs.

The aluminum mass balances for each of the Batch C regenera-
tions are summarized in Table 11.  Aluminum losses ranged
from 2.8 percent to 21.4 percent per cycle and averaged 8.7
percent during this series of runs.  Percentage loss was
calculated from the carbon loss equation presented earlier.

As can be seen from Figure 75, the aluminum/carbon ratio of
the regenerated slurry built up far beyond 0.027, the level
necessary for proper flocculation in the treatment process.
Excess alum was accidently added following the first and third
regeneration cycles accounting for a major part of the Al/C
ratio increases following these points.  Another source of
alum was makeup carbon to which was added 0.027 Ibs Al per
Ib carbon.

During the pilot runs, acidification of the regenerated carbon-
aluminum oxide slurry was carried out in 500 gallon tanks.
Sulfuric acid was added to the slurry which was rapidly mixed
and then a sample was withdrawn for a pH determination.
Additional acid was then added if required.  Using this method,
sulfuric acid requirements averaged 0.63 Ibs H2S04/ Ib carbon.

The acid usage during each regeneration cycle is shown in
Table 5 and Figure 76.  Acid requirements for regenerated
carbon are higher than for virgin carbon as is expected since
more acid soluble species exist in the regenerated slurry.
It appears that after one or two cycles, the acid requirement
is basically constant.

It was apparent that an excess of sulfuric acid was used in
the pilot studies because the method of acidification did
not lend itself to exact control of chemical dose.  If an
acidification technique utilizing more exact pH control were
employed, it should be possible to substantially reduce the
acid requirement.  Laboratory titrations of the regenerated
carbon slurries from the pilot operations indicate that it
should be possible to reduce the sulfuric acid usage to 0.5
Ibs H2S04/lb carbon.
STACK GAS SAMPLING

A stack sampling program was undertaken by the New York
State Department of Environmental Conservation, Division of
Air Resources.  All sampling was performed according to the
                          -121-

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                             TABLE  11


                 ALUMINUM MASS BALANCE SUMMARY


Regeneration Number	7	8	9	10	11	12_

Aluminum at End of
Previous Regeneration
      (Ibs)                          0   20.5  19.7   31.3    31.1   25.6

Virgin Aluminum Added at
End of Previous Regeneration
       (Ibs)                       28.0   7.5  16.8   13.5      0      0

Physical Losses in
Treatment System
       (Ibs)                        1.9   7.7    2.3   12.8     1.8    3.1

Aluminum Fed to
Regeneration Furnace
       (Ibs)                       26.1  20.3  34.2   32.0    29.3   22.5

Aluminum Recovered at
End of Regeneration                20.5  19.7  31.3   31.1    25.6   18.3
      (Ibs)

% Aluminum Loss
in Furnace                         21.4   3.0    8.5   2.8    12.6   18.7
                               -122-

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1
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NJ
U)
J
               0.08 -
               0.06 —
            
-------
             1.0
NJ
^
I
            0.2
                                              I
I
                                                                  O 1971 OPERATIONS

                                                                  A 1972 OPERATIONS
I
                                   2345
                                    NUMBER  OF  REGENERATION  CYCLES
                       FIGURE 76.   ACID USAGE DURING REGENERATION STUDIES

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EPA sampling method published in the December 23, 1971
Federal Register.  Tests were performed for nitrogen oxides,
sulfur oxides, water vapor, particulates, and trace metals.

Nitrogen oxide analyses were conducted on 5/9/72 using a
chemiluminescent analyzer.  During the test the firebox and
bed temperatures were 1780-1810°F and 1200-1300°F, respec-
tively.  The NO stack gas content was 48-50 ppm and the NC>2
concentration was 1-3 ppm.

The stack gas opacity was estimated to be 10-20 percent.
This was due to a large amount of steam and powdered carbon
in the stack gas at the time.

Samples for SO2 analysis were collected on 6/13/72.  No SC>2
was detected in the samples.

Stack samples for particulates, moisture content and trace
metals were collected 6/12-13/72.  The results are presented
in Table 12.  Particulate emissions are of major concern not
only because of the air pollution potential but because of
the loss of regenerated carbon which they represent.  The
relatively high particulate emissions in the stack gas
occurred as a consequence of the wrong size venturi being
supplied in the scrubber system.  Particle capture is a
function of the velocity through the venturi throat.  Since
the venturi throat was oversized in the pilot system,
particle capture was not highly efficient.  As can be seen
from inspection of the data of Table 12, during sampling runs
1 & 2 when the pressure drop across the venturi was 3.5-4 inches
of water, 1.8 to 1.5 percent of the carbon product was lost.
However, during run 3 when the pressure drop was increased
to 8.5 inches of water, the carbon loss was correspondingly
decreased to 0.92 percent.  Venturi manufacturers guarantee
that with a pressure drop of 20 inches of water, the maximum
particulate loss will be 0.078 Ib/hr, which corresponds to
0.67 and 0.54 percent carbon losses for runs 1 and 3, respec-
tively.  Since most of the furnace operation time was at the
conditions of run #1, the recoverable loss from the stack was
approximately 1 percent of the total carbon.

The carbon fraction in the stack gas particulates could not
be determined and therefore, the carbon/inert ratio in the
regenerated slurry was used to calculate stack carbon losses.
This will obviously underestimate the carbon loss since the
ash was mostly fine sand from the fluidized bed which is much
more readily captured by the cyclone type separator.  Since
the ash content of the stack particulates should be much
lower than the recovered carbon, the amount of carbon re-
coverable with a properly designed scrubber system is esti-
mated conservatively.
                          -125-

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      TABLE 12
STACK SAMPLING DATA
Sample Number
Bed Temperature, °F
Firebox Temperature, °F
Bed Velocity, ft/stc
Sludge Feed rate, Ibs/hr
Volume Sampled, scf
Moisture Content, %
Total Particulates, Ib/hr
Carbon, % of carbon feed
to furnace
Iron, Ibs/hr
1
1230
1830
1.7
80
43.3
37.2
0.213
1.84
0.00402
2
1250
1860
1.7
90
56.2
44.1
0.195
1.50
0.00313
3
1250
1840
2.2
100
66.0
51.4
0.189
0.92
0.000725
          -126-

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Thus installation of the proper sized venturi should sub-
stantially reduce carbon losses in the stack gases below the
measured levels.

CARBON REGENERATION STUDIES

The recovery of carbon from the regeneration furnace was
calculated on the basis of a fixed carbon mass balance over
the whole pilot plant.  The average carbon recovery over the
first four cycles was 89 percent per cycle.

Table 13 shows the breakdown of the carbon mass balance during
the 1972 portion of the study.  The carbon loss during the
period ranged from 1,3 percent to 22.3 percent.  The average
loss per cycle calculated on an overall basis was 9.7 percent.
Percentage loss was calculated by the equation
     % Loss =
Fixed Carbon Consumed - Physical Losses
  	- Fixed Carbon Recovered	
Fixed Carbon Consumed - Physical Losses
Overall  loss per cycle was determined by dividing the percentage
loss determined as  in the above equation by the total number
of regeneration cycles.

This method of loss calculation assumes that all physical
losses occurred during the sewage  treatment portion of the
pilot plant operation, prior  to regeneration.  Since small
losses did occur after regeneration, the percentage loss
figures  calculated  for each cycle  are slightly higher than
actual.

Carbon loss in the  stack gas  could not be routinely determined
and therefore, is not included in  Table 13.  As previously
discussed, the recoverable loss from the stack at typical
regeneration conditions was found  to be approximately 1 percent
of the carbon entering the furnace.  The remainder of the
carbon loss is attributed to  burning in the fluidized bed.
The carbon burned during regeneration is thus calculated
to be an average of 8.7 percent of the carbon entering the
furnace.

Determination of ash buildup  as the carbon was repeatedly
regenerated was complicated by the fact that some sand
was carried over from the furnace  and contributed to the
apparent "ash" content.  Sand carryover from the furnace
was collected with  the regenerated carbon in the scrubber
stream.   A portion  of this sand was separated from the
carbon slurry in the small settling chamber ahead of the
carbon storage tanks.  During runs 11 and 12 the average
amount of sand collected in this manner was 0.27 pounds per
pound of carbon recovered.  A significant quantity of sand
                           -127-

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                             TABLE 13


                   CARBON MASS BALANCE SUMMARY
 Regeneration Number               7    8    9    10     11     12


Fixed Carbon at
End of Previous Regeneration,
         (Ibs)                    --   687  499  828    504    468

Fixed Virgin Carbon Added
at End of Previous Regeneration
         (Ibs)                   787   131  498  157     0      0

Physical Losses in Fixed Carbon
in Treatment System
         (Ibs) '                   73   227   55 *336     30    57

Fixed Carbon Fed to
Regeneration Furnace
         (Ibs)                   714   591  942  649    474    411

Fixed Carbon
Recovered at End of
Regeneration Cycle
         (Ibs)                   687   499  828  504    468    356

% Carbon Loss in Furnace         3.8   15.6 12.1 22.3   1.3    13.4
*Approximately 300 pounds purposely wasted to reduce carbon
 inventory
                                -128-

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was not trapped in this manner and was cycled through the
system with the carbon.  Sieve analysis of the sand collected
in the settling chamber is  presented in Table 14.  As would
be expected the data show the sand to be very fine.

An efficient method of separating the fine sand and ash
from the powdered activated carbon is desirable in order to
reduce the amount of mass carried through the treatment and
regeneration systems.  A brief laboratory investigation was
conducted to study the feasibility of classification of the
carbon-inerts in the regeneration stream.  Fifty milliter
samples of the slurry from the seventh regeneration (Batch C)
were centrifuged for five minutes at various speeds corres-
ponding to radial accelerations up to 1350 gravities.  The
lower ten percent of the cake was then analyzed for inert
content with results as follows:

Radial acceleration, gravities    0    50    330   750   1350

Solids content of lower tenth, % 34.4  40.2  46.8  45.3  47.0

Inert content of lower tenth, %  52.2  70.3  78.5  78.3  77.7

The data show that at accelerations greater than 330 gravities
a cake is attainable which contains approximately 46 percent
solids of which 78 percent is inert material.  If this fraction
were wasted for blowdown, less than 22 percent of the blowdown
would be carbon thus  effecting a substantial savings in
carbon loss.  In addition, if the slurry were acidified prior
to the inert carbon classification, the loss of alum in the
blowdown would be reduced to only that portion dissolved in
the wasted slurry-

Based on these results, it appears that classification would
be feasible and could lead to reductions in operating costs
by reducing the carbon and aluminum lost to blowdown.

A number of factors must be considered in selecting the rate
of blowdown.  At a particular blowdown rate, the inert
material will eventually reach an equilibrium concentration.
This inert fraction will be cycled through the treatment
system, dewatered, and passed through the regeneration
system.  The costs associated with these operations increase
in proportion to the quantity of inert material carried.
However, a high rate of blowdown which would minimize the
quantity of inerts would increase carbon losses.  Therefore,
blowdown should be selected to minimize operating costs.

Based on the design and operating parameters presented in
Section VIII of this report, the effect of blowdown rate on
total treatment costs was calculated.  Two cases were assumed:
no classification and classification to achieve a blowdown
                          -129-

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                    TABLE 14
        SIEVE ANALYSIS OF FLUIDIZED BED SAND
         COLLECTED WITH REGENERATED CARBON
                      Weight              Fraction
                     Retained             Retained
Mesh                    (g)                  (%)

  40                    0.73                1.66
  50                     .42                0.96
  60                     .45                1.02
  70                     .40                 .91
 100                    5.20               11.83
 150                    7.84               17.84
 200                   20.22               46.01
Pan                     8.69               19.77

                       43.95              100.00
                       -130-

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stream containing 78 percent inerts.  The results are pre-
sented in Figure 77.  It is evident that classification would
significantly reduce treatment costs at optimum blowdown
rates.  In the case of no classification, optimum blowdown
would be 5 percent while with classification optimum blow-
down would be 6.5 percent.
                           -131-

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                       SECTION VIII


            DESIGN AND ECONOMIC CONSIDERATIONS
Based upon the data evolved in the Albany pilot plant
studies, preliminary estimates relating to design parameters
and the corresponding capital and operating costs for a 10
mgd treatment plant have been developed.  A conservative
approach was adopted in the development of these estimates
and therefore, they should represent a "worst case" — the
maximum probable costs — for a 10 mgd plant utilizing
the powdered carbon treatment process described in this
report.  For example, the tube settler loading rate utilized
in developing the capital cost estimates was the loading
rate actually used in the pilot studies.  The pumping
capacity of the pilot system and the operational problems
associated with the pilot tube settler prohibited investi-
gation of any higher loading rates.  It is probable that in
a commercial unit the loading rate could be increased sub-
stantially which would result in a reduction in capital
costs.  Therefore, further process development should lead
to a downward adjustment of capital and operating cost
projections.

Several major questions with regard to design of a commercial
fluidized bed carbon regeneration furnace require resolution
before an optimum, minimum cost system can be designed.  If
combustion could be carried out directly within the fluidized
bed chamber, the required unit area would be halved, the size
of the scrubber would be halved, and there would be no
requirement for a recycle blower.  However, this method of
operation might result in greatly increased carbon losses
through combustion.  At Albany, combustion was accomplished
in a chamber underneath the hearth and temperatures were
reduced to a practical limit by off gas recycle.  This latter
approach should be feasible for a commercial unit.  However,
there is a practical upper limit to the size of a brick
hearth which could be constructed.  Moreover, the combustion
chamber temperature cannot be raised above an upper limit
of 2000°F.

A substantial savings in capital and operating_costs can be
realized if off gases are not recycled.  The pilot program
utilized recycle, but earlier work by Battelle-Columbus<12)
indicated it may not be required.

Other potential cost savings lie in the area of waste heat
utilization.  Conceivably.- waste heat from the regeneration
                             -133-

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furnace could be used to dry the sludge before regeneration.
This would result in capital cost savings since a smaller
size furnace would be required.  In addition, fuel require-
ments would be reduced thus resulting in reduced operating
costs.

Classification of the carbon and inert fractions in the
regenerated stream prior to blowdown would reduce makeup
carbon and alum requirements.below those utilized for cost
projections in the current analysis.

For purposes of this report, two sets of conditions (off
gas recycle and no recycle) have been assumed and capital and
operating costs have been calculated for each case.  Costs
have been developed both for operation as municipal waste-
water and combined sewage treatment plants with two
configurations for each plant type.

SYSTEM DESIGN PARAMETERS

The design parameters used in developing the treatment system
capital cost estimates are given in Table 15.

SYSTEM CAPITAL COSTS

Capital costs are based on vendor information, published cost
data (12 ,13,14) ^ an(j engineering estimates of the required
equipment sizes.  Capital cost estimates for municipal waste-
water and combined sewage treatment are given in Table 16.

SYSTEM OPERATING PARAMETERS

Table 18 presents the system operating costs based on the
parameters presented in Table 17.

TOTAL SYSTEM COSTS

Total system costs include the operating costs given in
Table 18 plus amortization of the capital costs presented
in Table 16.  Amortization costs were calculated at 6 percent
over 25 years.  The total system costs are presented in
Table 19.
                             -134-

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                        TABLE 15
               SYSTEM DESIGN PARAMETERS
Treatment System

  Carbon Contact

     Time at pH 4
     Time at pH 7

  Flocculation

     Velocity Gradient
     Time

  Tube Settler Loading Rate

  Filter

     Length of Filter Run
     Loading Rate

  Chlorine Contact Time

  Chemical Storage Capacity

  Sludge Storage

Regeneration System


  Combustion Chamber Temperature, °F

  Bed Temperature, °F

  Fluidizing Gas Velocity, ft/sec

  Heat Requirement, million BTU/hr

  Bed Diameter, 2 units, each, ft

  Slowdown, %
   10 minutes
    5 minutes
   75 fps/ft
   10 minutes

 2880 gpd/ft2
   12 hour s
    5 gpm/ft2

   10 minutes

   12 hours

    1 day

With gas   Without
 recycle  gas recycle
  2000

  1250

   1.3

  30.7

  21.7

   5
2000

1250

 1.0

24.5

19.8

 5
                          -135-

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                               TABLE 16
             CAPITAL COST ESTIMATES FOR 10 MGD MUNICIPAL
             WASTEWATER AND STORM WATER TREATMENT PLANTS
                               Municipal Plant       Storm Water Plant
Item                           Installed Costs, $    Installed Costs, $
Screens,  grit chamber,
  overflow                         10,000                10,000
Reaction vessels                   27,000                27,000
Chemical storage tanks              32,000                32,000
Carbon slurry tanks                40,000                40,000
Sludge storage                     17,800                17,800
Pumps                              35,000                35,000
Agitators                          45,700                45,700
Flocculation, sedimentation       475,000               475,000
Filtration                        300,000                 	
Chlorination                       14,700                14,700
Centrifuge                         80,000                80,000
Sludge pumps                       53,700                53,700
Regeneration facility
     With gas recycle           1,104,000                 	
     Without gas recycle          794,800               794,800
     Subtotals
      With gas recycle           2,234,900                 	
      Without gas recycle       1,925,700             1,625,700
      Without regeneration          	                 830,900
     Total Capital Costs*
      With gas recycle           2,462,390                 	
      Without gas recycle       2,121,270             1,791,270
      Without regeneration          	                 966,990
Contingencies 10%
 Land, 1.5 acres @ $2000/acre
                                  -136-

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                                                    TABLE 17
                                           SYSTEM OPERATING PARAMETERS
H1
u>
       ITEM
       Treatment  System
           Carbon  dose,  mg/1
           Alum  dose, mg/1
           Polyelectrolyte  dose,  mg/1
           Lime  dose, mg/1
           Sulfuric acid,  #/t carbon
     Sludge dewatering polyelectrolyte
       dose, f/ton dry solids
Regeneration System
     Carbon recovery, %
     Alum recovery, %
     Slowdown, %
     Carbon feed rate, f/hr
     Sludge feed rate, #/hr
     Sludge solids content, %
     Sludge inerts content
       % on dry basis
     Fuel, C/MBTU
                          /
     Power, C/kwhr
     Slowdown disposal cost, */lb solids
                                                    MUNICIPAL
                                                      PLANT
                                                600
                                                200
                                                2.0
                                                150
                                                0.5
                                                                                STORM WATER PLANT
                                                       91
                                                       91
                                                        5
                                                      2080
                                                     21,800
                                                       22

                                                       60
                                                       25
                                                       0.7
                                                       0.4
With Regeneration
400
200
2.0
150
0.75
1
91
91
5
1390
21,800
22
60
25
0.7
0.4
Without Regeneration
400
200
2.0
	
	
1
0
0
100
—
	
—
	
25
0.7
0.4

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                                                   TABLE 18
                                OPERATING COST ESTIMATES FOR 10 MGD MUNICIPAL
                                 WASTEWATER AND STORM WATER TREATMENT PLANTS
OJ
co
      ITEM
Sulfuric acid
Lime
Make-up alum
Polyelectrolyte
Make-up carbon
                   2
Carbon regeneration
  With gas recycle
  Without gas recycle
Slowdown Disposal
Chlorination
Power
Labor, 60 hr/day @ $4.00/hr
TOTAL
  Regeneration with gas recycle
  Regeneration without gas recycle
  Without regeneration

  Includes dewatering dose
  Includes fuel costs
3 40 hr/day
                                             MUNICIPAL
                                                With
                                            Regeneration
                                             C/1000 gal
                                               4.3
                                               0.8
                                               0.7
                                               2.9
                                               6.3
                                               3.5
                                               2.9
                                               0.2
                                               0.2
                                               0.2
                                               2.4
                                              21.5
                                              20.9
                                                                STORM WATER
With
Regeneration
C/1000 gal
4.3
0.8
0.7
2.9
4.2
_ „„
2.9
0.2
0.2
0.2
2.4
Without
Regeneration
C/1000 gal
0
0
5.0
2.9
30.1
0
0
0
0.2
0.2
1.63
18.8
                                                                                 42.9

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                                      TABLE 19


                          TOTAL COSTS FOR 10 MGD MUNICIPAL
                     WASTEWATER AND STORM WATER TREATMENT PLANTS


PLANT DESCRIPTION                  OPERATING COST     AMORTIZATION COST       TOTAL
                                     C/IOOO gal          C/IOOO gal         C/IOOQ qal

Municipal, with gas recycle             21.5               5.11               26.6

Municipal, without gas recycle          20.9               4.58               25.5

Storm, without regeneration             42.9               1.84               44.7

Storm, regeneration without
  gas recycle                           18.8               3.43               22.2

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                      SECTION IX


                   ACKNOWLEDGMENTS
The authors wish to extend their gratitude to the many
people whose assistance was necessary to the timely and
successful completion of this program.  A. T. Brix, J. J.
Dorgan, and J. Green made significant contributions to the
pilot plant design.  R. G. Parkhurst and M. J. Mason
contributed significantly of their own time during the
pilot plant shakedown at Richland.  Battelle's operating crew
at Albany, J. A. Coates, M. J. Mason, R. G. Swank, and R. G.
Upchurch invested many long hours in keeping the plant
operating and contributed in large part to the success of
the Albany demonstration.  Other Battelle personnel who
contributed advice, suggestions, time, and moral support
throughout the course of this program include B. W. Mercer
and D. E. Olesen.  Former Battelle personnel who also fall
in this category are Dr. C. J. Touhill and Mr. G. L. Gulp.

Mr. Danforth Bodien and Mr. Frank Condon of the Environ-
mental Protection Agency provided support and assistance
throughout the course of this program.

Nichols Engineering and Research Corporation designed and
supplied the fluidized bed pilot regeneration furnace used
in the study.  Mr. Charles von Dreusche, Jr. provided much
assistance in overcoming problems with the unit and
developed much of the furnace cost data used in this report.
Mr. George Nowowiejski, also of Nichols, invested much time
and effort during the shakedown of the furnace.

Dr. Leo Hetling of the New York State Department of Environ-
mental Conservation provided assistance in locating and
obtaining the Albany site.  He also provided help in numerous
ways throughout the operations at Albany and has initiated
studies by the New York State Department of Environmental
Conservation to characterize the Island Creek Drainage Area.

Mr. Walter Connley of Neptune Microfloc, Inc., provided
cost information used in this report.
                           -141-

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                       SECTION X
                       REFERENCES
 1.   "Problems of Combined Sewer Facilities and Overflows."
      Federal Water Pollution Control Administration, U. S.
      Department of Interior, WP-20-11.1967.

 2.   Weibel, S. R., Anderson, R. J., and Woodward, R. L.
      "Urban Land Runoff as a Factor in Stream Pollution,"
      J. Water Pollution Control Federation, Vol. 36, pp.
      914-924.1964.

 3.   Burns, R. J. , Krawczyk, D. F., and Harlow, G. L.
      "Chemical and Physical Comparison of Combined and
      Separate Sewer Discharges."  J. Water Pollution Control
      Federation, Vol. 40, pp. 112-126.  1968.

 4.   "Water Pollution Aspects of Urban Runoff."  Federal Water
      Pollution Control Administration, U. S. Department of
      Interior, WP-20-15.  1969.

 5.   Shuckrow, A. J., Dawson, G. W., and Olesen, D. E.  "Treatment
      of Raw and Combined Sewage . "  Water and Sewage Works,
      pp. 104-111.  April 1971.

 6.   Rizzo, J. L. and Schade, R. E.  "Secondary Treatment with
      Granular Activated Carbon."  Water and Sewage Works,
      p. 307.  1969.

 7.   Weber, W., Hopkins, C. B. and Bloom, R.  "Physiochemical
      Treatment of Wastewater."  Journal Water Pollution Control
      Federation, p. 83.  1970.

 8.   Zuckerman, M. M. and Holof, A. H.  "High Quality Reuse
      Water by Chemical-Physical Wastewater Treatment."  Journal
      Water Pollution Control Federation, p. 437.  1970.

 9.   Shuckrow, A. J., ejt al.  "A Pilot Study of Physical-
      Chemical Treatment of the Raw Wastewater at the Westerly
      Plant in Cleveland, Ohio."  A paper presented at the
      International Association on Water Pollution Research
      Workshop, Vienna, Austria.  September 1971.

10.   "Standard Methods for the Examination of Water and
      Wastewater."  Twelfth and Thirteenth Editions, APAA,
      AWWA, WPCF.  1967 and 1971.
                            -143-

-------
11.  Berg,-  E.  L.,  ejt al.   "Thermal Regeneration of Spent
     Powdered  Carbon Using Fluidized-Bed and Transport Reac-
     tors."  Chemical Engineering Progress Symposium Series
     No.  107,  Vol.  67.   1971.

12.  "The Development of  A Fluidized Bed Technique for the
     Regeneration  of Powdered  Activated Carbon."  Water
     Pollution Control  Research Series, 0RD-1707OFBD03/70,
     Federal Water  Quality Administration.  1970.

13.  Gulp,  R.  L. and G. L.  Gulp.   "Advanced Wastewater
     Treatment." Van Nostrand  Reinhold, 1971.

14.  Guthrie,  K. M.   "Capital  Cost Estimating." Chem.  Engr.,
     Vol.  76,  No.  6.  March 24,  1969.
                          -144-

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                      SECTION XI


                      APPENDIX A


                  LABORATORY STUDIES


An extensive laboratory program to develop and establish
the feasibility of the physical-chemical treatment process
described in this report was carried out from July 1969
through March 1970.  The results of this laboratory program
are described below.

GENERAL

Influent to the Richland, Washington, sewage treatment plant
was used in all of the laboratory work.  At the outset of the
investigation, an extensive analytical study to characterize
Richland sewage was carried out in order to investigate the
suitability of this influent for use in the laboratory
studies on the treatment process.  Grab samples were obtained
at various times of the day over a 3-1/2 day period and were
analyzed for various constituents in accordance with the
procedures outlined in "Standard Methods*^' .  Ca and Mg
concentrations were determined by atomic absorption tech-
niques.  The results of the characterization are presented
in Table A-l.

During the course of the research, a Beckman Model 915 Total
Organic Carbon Analyzer was obtained and when this instru-
ment became operational, TOC measurements were substituted
for COD determinations.

A bench scale continuous flow system was constructed early
in the program.  As the work progressed, this system was
modified several times to incorporate features such as in-
line mixing and pH control.  Two basic types of clarifiers
were employed in this system: a tube settler and an upflow
clarifier.  Upon selection of tube settlers for the pilot
plant„ all further bench scale work was conducted with the
laboratory tube settler.  Figure A-l is a schematic diagram
of the final laboratory system.

CARBON STUDIES

Aqua Nuchar A was selected for use in initial studies based
on its relatively low cost and satisfactory performance in
prior studies.  Several sets of experiments were conducted
to examine the sorption characteristics of the powdered
carbon.  In order to accomplish this, 300 ml aliquots of
fresh Richland influent were placed in 8 oz polyethylene
                           -145-

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           TABLE A-l
COMPOSITION OF HIGHLAND SEWAGE
Time of
Day
Conductivity
(ymhos/cm)
PH
Temp °C
Turb (JTU)

Alkalinity
(mg/1 as CaCO3)
Ca (mg/1)
Mg (mg/1)
COD (mg/1)
NH.-N (mg/1)
4
NO -N (mg/1)
2
0700
950-620
750-6
7.68-7.47
7.56-6
22-20
21-2
28-10
19-2
252-199
239-6
43-36
40-4
13-10
11.5-4
160-130
142-6
20.7-10.8
15.3-6
.22-. 01
.067-5
1130
1600-820
1080-4
7/72-7.60
7.69-4
26-25
25.5-2
105-68
87-2
325-297
310-4
45-38
41-3
15-10
12-3
544-436
503-4
44.8-32.7
39.4-4
.025-. 01
.019-4
1620
460-400
430-3
7.48-7.36
7.42-3
26
26-2
130-90
110-2
264-224
248-3
41-38
40-3
12-9
10-3
525-267
351-3
19.9-14
17-3
.01-0
.003-3
1930
532-460
490-3
7.36-7.30
7.33-3
24-22
23-2
150-55
103-2
254-229
248-3
44-36
40-3
12-8
11-3
525-303
401-3
17.5-13.2
15.5-3
.025-0
.012-3
2340
590-540
567-3
7.38-7.31
7.34-2
24-23
23.5-2
160-58
109-2
277-253
267-3
45-43
44-2
12
12-2
450-400
431-3
21.8-18.3
20.1-3
.025-0
.012-3
          (continued)

-------
     TABLE A-l  (continued)




COMPOSITION OP HIGHLAND  SEWAGE
Time of
Day
NO3-N (mg/1)
Org. N
Sol P04
(mg/1)4
TS (mg/1)
TVS (mg/1)
SS (mg/1)
VSS (mg/1)
Settleable Solids
(ml/1)
Settleable Solids
(mg/1)
NOTE: Numbers for
0700
3.2-0
.66-6
17.1-6.7
11.6-6
41-20
30.1-6
1080-510
705-6
261-168
204-6
124-51
93-5
93-5
92-30
60-5
4.0-3.5
3.7-3
145-82
114-2
each time
1130
.15-. 10
.11-4
31.7-12.6
21-4
34-27.5
31-4
894-694
764-4
474-329
400-4
320-228
274-4
274-4
208-176
188-4
15-11.5
13-3
315-148
232-2
period represent:
1620
.02-0
.007-3
12.6-10.2
11.8-3
50-26.5
38.8-3
735-636
685-2
303-234
294-3
286-198
219
219-3
164-122
139-3
9-5
7.1-3
180-52
116-2
1930
.2-0
.13-3
13.9-9.4
11.6-3
34.5-30.
33.3-3
724-672
701-3
454-319
375-3
315-168
232-3
182-103
151-3
17-5.5
9.8-3
278-112
204-3
J high value - low
[average - no. of
2340
.2-0
.1-3
12.5-11.7
12.2-3
5 37.5-31.5
35.1-3
770-685
721-3
450-363
418-3
275-165
211-3
203-112
173-3
8-7
7.3-3
191-164
178-2
value \
samples]

-------
                                        .IME  SLURRY
1
I—1

oo
                                                                                    FEED
                                                                                    PUMP
             CHEMICAL  FEED  PUMPS
                                      CARBON-ALUM  FEED
                                                                               SEWAGE
                                                                                FEED
                                                                                TANK
                        SLUDGE  WITHDRAWAL
                                  FIGURE A-l,  BENCH SCALE  SYSTEM

-------
bottles and a quantity of powdered carbon was added to each
bottle.  The set of samples was then placed on a mechanical
shaker and was agitated overnight.  This was believed to be
a sufficient period in which to establish equilibrium con-
ditions.  Each carbon-sewage mixture was then filtered
through a 0.45 y membrane filter and the COD of the filtrate
was determined.  Figure A-2 contains the results for seven
different sewage samples.  It appears that sorption of COD is
essentially complete at a carbon concentration of 800-1000 mg/1.
Increasing the carbon concentration beyond this point has little
or no effect on the residual COD.  Two parallel sets were run in
one instance in order to determine if the presence of bentonite
had any effect on t'he sorption equilibrium.  As seen from in-
spection of Figure A-2, 300 mg/1 of bentonite had no noticeable
effect on the equilibrium solution concentration of COD.

Sewage samples were contacted with 1000 mg/1 of Aqua Nuchar A
for various time intervals and were then centrifuged and finally
filtered through 0.45 v filters.  COD analyses of the filtrate
indicated that sorption was essentially complete after a con-
tact period of ten minutes.  Subsequent to these findings, a
carbon concentration of 1000 mg/1 and a contact time of ten
minutes were adopted for experimental use.

Subsequent tests, run with 500 ml sewage aliquots and one
hour contact times, suggested that TOC removal is virtually
complete at a carbon dose of 500-600 mg/1.  Data from these
tests are presented in Figure A-3.  In view of these findings,
another series of tests to examine required detention time
at the lower carbon dose was conducted.  As can be seen from
inspection of the data in Figure A-4, a ten minute detention
time should be adequate even at this reduced carbon dose.

Subsequently, samples of fifteen different commercial grade
powdered carbons were evaluated in a series of tests.  Earlier
comparisons showed little or no correlation between methylene
blue adsorption and organic carbon removal.  Hence, tests were
based on residual organic carbon concentrations after both
contact tests and jar tests.

Contact tests were conducted using 500 ml sewage samples
dosed to 1000 mg C/l.  Duplicate samples were prepared,  one
of which was shaken for an hour and the second for 21 hours.
The samples were then filtered through 0.45 p membrane
filters and analyzed for total organic carbon.   This pro-
cedure was repeated for seven of the carbons with a sewage
sample obtained on a different day.  The results of these
runs are given in Table A-2.

Based on the results of the contact tests, selected carbon
types from the different companies were used in jar tests.
A carbon dose of 1000 mg/1 was used with 350 mg/1 alum
                           -149-

-------
  80
  70
  60
  50
o-
LU
  40
  20
  10
        X
        V
        o
        A
        A
        D
INF
INF
INF
INF
INF
INF
INF
INF
A SET
A SET
B
C
C*
D
E
F
#1
#2
       CONTACT  TIME  =  18  HOURS
      *WITH  300 mg/£ BENTONITE
       ADDED
              1000    2000    3000   4000
              CARBON CONCENTRATION  (mg/O
                          5000
     FIGURE A-2.
EFFECT OF CARBON CONCENTRATION
      ON EQUILIBRIUM COD
                        -150-

-------
   120
   108
    96
   84
   72
5- 60
UJ
P.  48


UJ
I—

OL

^  36
i—i
Ll_




   24







   12
                O INF 1
                a INF 2
                A INF 3

              CONTACT TIME = 1 HOUR  -
         I
                     I
         0     400    800     1200    1600
          CARBON CONCENTRATION  (mg/£)
    FIGURE A-3.
EFFECT OF CARBON CONCENTRATION

      ON EQUILIBRIUM TOC
                        -151-

-------
120
                            o   600 mg/£ AQUA NUCHAR A
                               1000 mg/£ AQUA NUCHAR A
                    10      15       20
                    CONTACT TIME (WIN)
30
 FIGURE A-4.  EFFECT OF CONTACT TIME ON TOC REMOVAL


                        -152-

-------
                         TABLE A-2
        COMPARISON OF VARIOUS CARBONS - CONTACT TESTS

TOC
Sample 1 hr
Nuchar CEEN
Darco S51
Nuchar WAN
Nuchar C190A
Nuchar C115N
Nuchar C115A
Nuchar Aqua
Nuchar C190N
Pittsburgh GW
Nuchar CEEA
Nor it FQA
Darco GFP
Whitco 517
Darco KB
Norit F
Sewage A
(mg/1) TOC
contact 21 hr
7
8.5
8.5
9
10
10
10.5
11
11.5
13.5
15
16
16.5
16.5
17

(mg/1)
contact
7
12
9
7
10.5
9.5
7
12
7
8
9.5
10
11
11
12
Sewage B
TOC (mg/1)
1 hr contact
7.5
14.5
9.5
10.5
—
12.5
10.5
—
10.5
—
—
—
--
—

Bulk
Cost
(*/#)
14
13
10.5
15.5
15.5
13.5
9
15.5
15.5
14
12.5
10.5
—
29
11.5
Sewage A Soluble TOC =35.5 mg/1



Sewage B Soluble TOC =47.5 mg/1




Carbon Dose = 1000 mg/1
                             -153-

-------
added after 5 minutes contact time and 10 mg/1 of Magnifloc
985 N added after an additional 5 minutes.  Samples were
then flocculated, allowed to settle, and the unfiltered
supernatant was analyzed for organic carbon as before.
Results for two different sewage samples are given in
Table A-3,  together with several qualitative observations
on wettability and floe characteristics.

Based on these findings, the decision was made to continue
using Aqua Nuchar A since it appeared to offer the best
benefit/cost ratio.                            i

BENTONITE PROCESS DEVELOPMENT

Preliminary investigations prior to the start of the project
indicated that bentonite clay,  in conjunction with a poly-
electrolyte, could effectively coagulate powdered carbon.
Based on these preproject findings, Magnifloc 985 N, a high
molecular weight, nonionic,  polyacrylamide was selected for
use in the early work.

A series of jar tests was conducted to determine the effect
of bentonite concentration on the flocculation-sedimentation
characteristics of the system with the results given in
Figure A-5.  When no bentonite was added to the system, large
quantities of carbon remained in suspension at the end of the
five minute settling period.  Although it is not obvious
from Figure A-5, the flocculation-sedimentation character-
istics of the system noticeably improved up to a bentonite
concentration of 300 mg/1.  However, the five minute settling
period was sufficient to effect good phase separation at a
bentonite dose of 100 mg/1.   This result was also observed
when the polyelectrolyte dose was reduced to 5 mg/1.  Simul-
taneous addition of bentonite and carbon to the system had
no detectable effect on COD removal or flocculation.  The pH
of the system was varied from 5.5-8.1 and no significant
change in system performance was observed.  Turbidity of
the settled effluent consistently ranged from 5-13 JTU.
Upon filtration of these effluent samples, the residue on
the membrane filter appeared to be clay rather than carbon.

These promising results prompted the initiation of an investi-
gation of the effectiveness  of  the process in a continuous
flow system.  Table A-4 summarizes the data of five runs with
the tube settler system.  Carbon,  bentonite and polyelectro-
lyte concentrations were set at 1000 mg/1, 300 mg/1, and
10 mg/1, respectively, in the initial runs to study the effect
of variable flow rates.  It  was realized that these concentra-
tions represented an excess  of  polyelectrolyte and probably
bentonite as well.

It appeared that the bentonite  dose could be reduced to 100-
200 mg/1.  In general, the bentonite process seemed to produce
                           -154-

-------
                             TABLE A-3
              COMPARISON OF VARIOUS CARBONS - JAR TESTS
Sample
Whitco 517
Pittsburgh GW
Darco S51
Nuchar CEEN
Nuchar Aqua
Nuchar WAN
Influent
TOC
(mg/1)
9.5
9
11.5
12
15.5
11.5
47.5
TOC
(mg/1)
14.5
20.5
16.5
35.5
32.5
17.5
75.5
Floe
Good
Good
Good
Fair
Good
Fairly Good
--
Wettability
Good
Average
Good
Average
Average
Average
--
Carbon Dose = 1000 mg/1
                               -155-

-------
  100
   80
   60
Q
O
O
   40
   20
         O BENTONITE ADDED
           FOLLOWING 10 MINUTE
           CARBON CONTACT
         • CARBON AND BENTONITE
           ADDED SIMULTANEOUSLY
                CARBON CONC.-1000 mg/£
                MAGINIFLOC 985 =10
                UNFILTERED SAMPLES
                          I
              100       200       300
             BENTONITE CONCENTRATION
                             400
   FIGURE A-5.
EFFECT OF BENTONITE CONCENTRATION
       ON EFFLUENT QUALITY
                       -156-

-------
                                                  TABLE A-4


                              BENCH SCALE SYSTEM OPERATIONAL  DATA - TUBE SETTLER
I
M
Ul

I
Date Influent Influent Flow
COD S.S. Rate*
(mg/1) (mg/1) (ml/min)
8/25/69 84 71
8/26/69 169 195
8/27/69 184 134
8/28/69 202 192
8/29/69 400 239
*Flow rates are listed in the
of 100 ml/minute represents
195
195
100
100
48
48
100
150
200
200
285
285
300
300
300
300
100
100
100
200
200
200
200
200
200
200
200
300
order in
a loading
Carbon Bentonite Polyelectrolyte Effluent Effluent
Cone. Cone. Cone. S.S. COD
(mg/1) (mg/1) (mg/1) (mg/1) mg/1)
1000
1000
1000
1000
1000
1000
1000
1000
1000
1000
1000
1000
1000
1000
1000
1000
1000
1000
1000
1000
1000
1000
1000
1000
1000
1000
1000
1000
which they
rate of 4 .
300
300
300
300
300
300
300
300
300
300
300
300
300
300
300
300
300
300
300
0
50
100
150
200
300
300
100
100
were vari
84 gpm/ft2
10
10
10
10
10
10
10
10
10
10
10
6.
0.
2.
5.
7.
0.
3.
7.
10
10
10
10
10
10
5
5
5
ed during
of tube
18
20
18
16
18
14.
44
18
50
50
45
7 30
5 290
5 57
0 35
5 43
75 51
75 43
5 35
117
51
51
44
26
28
13
11
a particular run.
surface.
18
12
12
11
13
14
46
38
56
42
46
46
96
37
20
23
18
17
11
174
70
49
57
45
28
31
42
24
A flow
COD
Removal
(%)
66
77
77
79
75
73
73
77
67
75
73
73
48
80
8°
88
90
90
94
14
65
76
72
78
86
92
89
94
rate

-------
a higher quality effluent in the continuous flow system than
in the jar tests.  Some further increase in flow rate may have
been possible, but it was believed that the 300 ml/min flow
was near the limit of the system without carbon carryover.
This limitation was due to the sizing of the tube settler.
The one inch diameter tube settler was a standard laboratory
model purchased from Neptune MicroFloc Inc.  At a system
flow rate of 100 ml/min, the throughput rate of the tube
settler was 4.84 gpm/ft^.

An additional six runs were conducted with an upflow clarifier
system.  Flow rates were varied from 300-1500 ml/min, giving
a range of system detention time from 62-12 minutes.  Chemical
doses were held constant at 300 mg/1 bentonite, 1000 mg/1
carbon, and 10 mg/1 Magnifloc 985 throughout the runs. Results
of these runs are summarized in Table A-5.  Turbidity of the
effluent ranged from 3.1 JTU at a flow rate of 300 ml/min,
to 6.2 JTU at a flow rate of 1500 ml/min.  As described later
in this section, carbon-bentonite sludges were regenerated by
Battelle-Columbus and by FMC Corporation.  Jar test evaluations
of the regenerated products revealed that the coagulating
ability of the bentonite was destroyed to a considerable
degree in the regeneration process.   Apparently, thermal
treatment causes the bentonite structure to collapse and
this alteration renders it inoperable as a coagulant.

It was found necessary to add a full 300 rng/1 of fresh
bentonite to the regenerated carbon-bentonite mixtures in
order to achieve good coagulation.

Even with the addition of new bentonite, the effluent had
poor turbidity characteristics in comparison to the effluent
produced using virgin carbon and bentonite.  It is postu-
lated that this was caused by the colloidal suspension of
spent bentonite ash.  Good clarification requires the addition
of other flocculant aids.

A screening study was conducted in an attempt to find a
suitable substitute for bentonite.  Materials which were
investigated and rejected include aluminum silicate, syn-
thetic zeolite, diatomaceous earth,  powdered silica, and
asbestos.

Bentonite does not appear to offer much promise if thermal
regeneration is to be utilized.  It would probably be
possible to recycle the carbon-bentonite mixture several
times.  However, buildup of the inorganic content will be
severe, and frequent wasting of large quantities of carbon-
bentonite would probably be required.
                           -158-

-------
          TABLE A-5
UPFLOW CLARIFIER OPERATING DATA
Flow
Rate
(ml/min)
300
350
600
700
1500
Overflow
Rate
(gpm/ft2)
0.189
0.220
0.378
0.441
0.945
Number
of
runs
5
1
5
1
3
Influent COD
(mg/1)
Range Avg
213-259 206
	 247
213-259 209
	 247
213-259 196
Effluent COD
(mg/1)
Range Avg
7-33 17
10-16 13
9-46 19
41-45 43
22-38 28
COD
Range
85-94
93-96
82-96
82-84
81-87
Removal
Avg
92
95
91
83
84

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ALUM PROCESS PRELIMINARY INVESTIGATIONS

Magnifloc 985 N was used throughout these initial investiga-
tions as was a carbon dose of 1000 mg/1.  The alum [Al2(804)3
= 181*20]  dose was varied in a series of jar tests.  From in-
spection of the data of Figure A-6 it is apparent that adequate
turbidity removal was achieved at an alum dose of 150 mg/1.
However, objectionable quantities of powdered carbon remained
in the effluent and good flocculation was not achieved until
the alum dose had been increased to 350 mg/1.  Additional
jar tests at this alum concentration and at polyelectrolyte
concentrations of 5-10 mg/1 indicated that COD removals of
>90% could be obtained consistently.  It was observed that
coagulation was impaired in some instances if alum and carbon
were added simultaneously.  A carbon contact time of at least
five minutes prior to alum addition was required in order to
insure consistently good floe formation.

Bench scale experiments with the alum process were then
conducted.  As indicated by the jar tests, a definite
carbon contact time of at least five minutes was required
before addition of the alum for coagulation to proceed
normally.  Data from runs with the upflow clarifier and the
tube settler are presented in Tables A-6 and A-7.

In the first two of the runs with the tube settler, numerous
mechanical difficulties with pumps, mixers, etc., arose.  Due
to the low flow rates employed, the system was slow to reach
equilibrium.  Therefore, the data reported for these first
two runs does not represent optimum system performance but
does indicate that even during minor upsets, a reasonable
degree of treatment can be achieved.  Tube settler performance
was similar to that observed for the bentonite system:
settling occurred primarily in the inlet chamber.  The floe
formed in this process was not as dense nor as tough as that
formed with bentonite.  Therefore, it was necessary to exer-
cise greater care to prevent breakup of the floe and redisper-
sion of the carbon after polyelectrolyte addition.

CARBON REGENERATION

An arrangement was made with Battelle-Columbus (BCL)  and with
FMC Corporation to regenerate a number of samples in their
respective laboratory carbon regeneration systems.  The initial
carbon-bentonite sludge sample sent to FMC was generated in
the laboratory bench scale unit.  All of the sludge samples
sent to BCL and the second set of FMC samples were generated
by treating a larger quantity of sewage on a batch basis.
Each set of sludge samples was generated by treating six
hundred gallons of sewage in batches of 50 gallons.  Half
was treated using the bentonite process and half by the alum
process.  After initial separation, the sludge was allowed to
                           -160-

-------
                       CARBON  DOSE  =  1000  mg/£
                       MAGNIFLOC  985  =  10  mg/£
       100
   200      300      400
  ALUM  DOSE  (mg/M
500
FIGURE A-6.
EFFECT OF ALUM DOSE ON COD
   AND TURBIDITY REMOVAL
                 -161-

-------
                                         TABLE  A-6
                    UPFLOW CLARIFIER SYSTEM - ALUM PROCESS PERFORMANCE
Influent
COD
(mg/1)
180



324

Flow
Rate
(ral/min)
600
600
300
300
600
300
Overflow
Rate „
(gpm/ft: )
0 .378
0.378
0.189
0.189
0.378
0.189
Alum*
Cone .
(mg/1)
400
350
350
350
350
350
Polyelectrolyte
Concentration
(mg/1)
10
19
10
5
4
5

SS
(mg/1)
13
19
13
16
36
18
Effluent
Turbidity
(JTU)
2
1.5
111
1
5.1
2.5

COD
(mg/1)
12
8
4
13
38
26
COD
Removal
%
93.4
95.6
97.5
93
88
92
*Alum - A12(S04)3-18H20




Carbon Dose = 1000 mg/1

-------
                                       TABLE A-7
                           TUBE SETTLER SYSTEM - ALUM PROCESS
Influent
COD TOC
(mg/1) (mg/1)
280 46
i
H>
Y* 188 73
>800 86

186 66

Flow Rate
(ml/min)
150
200
150
200
150
250
250
300
Tube
Loading Rate
(gpm/ft2)
7.26
9.68
7.26
9.68
7.26
12.10
12.10
14.52
Effluent
S.S.
(mg/1)
14
9
11
16
20
9
13
13
Turbidity
(JTU)
2.1
1.6
3.0
2.5
2.0
1.5
3.0
4.0
COD
(mg/1)
70
36
28
53
53
57
32
19
TOC
(mg/1)
8.0
8
4.5
11.5
-
9
21
Removal
COD TOC
76
87
85
72
>93
>93
83
90
81.5
82.6
93.8
86.6
—
86.3
46
Carbon dose - 1000 mg/1
Alum dose = 350 mg/1
Polelectrolyte dose = 10 mg/1

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concentrate for several hours,  the supernatant liquid was
poured off, and this procedure  was repeated a second time.
In most cases,  the dewatered sludge was oven dried before
shipment.  Physical losses in handling these small quantities
of carbon were significant in both cases and therefore it is
difficult to estimate the processing losses involved in
either system.   In fact,  these  handling losses were so high
that large quantities of  makeup carbon had to be added after
each regeneration cycle.   Therefore, an exact picture of
several cycles of use and reuse could not be obtained.

Carbon was followed through three regeneration cycles for
the Battelle-Columbus process.   The carbon composition of the
sludge regenerated in each cycle was as follows:
First Cycle - Bentonite Process
              Alum Process

Second Cycle- Bentonite Process
              Alum Process
Third Cycle - Bentonite Process
              Alum Process
100% Virgin carbon
100% Virgin carbon

75% First cycle regenerated
    carbon
25% Virgin carbon
50% First cycle regenerated
    carbon
50% Virgin carbon

66% Second cycle
    regenerated carbon

55% Second cycle
    regenerated carbon
45% Virgin carbon
Samples of the various regenerated carbon mixtures were analyzed
for carbon, water, and ash content with the results given in
Table A-8.  It should be noted that the ash content reading
includes the alum and bentonite residue except in the case of
the acid extracted carbon.  These data show how the bentonite
content of the sludge from the bentonite process increases
with each cycle.  An ash content of 44 percent was measured
after the third regeneration.   On the other hand, the compo-
sition of the acid extracted carbon-alum mixture is comparable
for the second and third cycles.  Definite conclusions con-
cerning physical losses and ash buildup in the alum process
could not be drawn on the basis of the laboratory studies.
Carbon contact tests were employed to determine the capacity
recovery of the carbon after regeneration.  The aluminum-
containing mixtures were slurried overnight at a pH of 0.5
to dissolve all soluble aluminum.  The dried powders, re-
generated bentonite-carbon, and new Aqua Nuchar were then
measured out at 0.5, 0.75, 1.0 and 1.5 gm/litcr for contact
tests.  Samples were shaken for one hour, filtered through
                           -164-

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                             TABLE A-8


              ANALYSIS OF REGENERATED CARBON MIXTURES
                     Carbon Content   Water Content   Ash Content
Virgin Aqua Nuchar
1
2
3
BCLA
1st Cycle
2nd Cycle
3rd Cycle
ABCLA
1st Cycle
2nd Cycle
3rd Cycle
BCLB
1st Cycle
2nd Cycle
3rd Cycle
FMCA
1st Cycle
AFMCA
1st Cycle
FMCB
Batch Scale
1st Cycle

84.1
.86.6
83.6

81.6
75.2
73.0

--
68.3
67.6

69.7
60.0
53.5

66.6

60.7

65.1
81.6

9.0
4.5
10.8

6.8
7.2
6.1

—
13.5
16.2

5.7
1.8
4.5

2.7

11.7

3.6
2.3

2.4
2.3
1.7

12.5
17.5
19.8

--
8.2
7.4

25.2
37.6
44.2

29.3

22.4

32.1
15.5
BCLB  - Regenerated carbon-bentonite mixture - Battelle-Columbus
        process
BCLA  - Regenerated carbon-alum mixture - Battelle-Columbus process
ABCLA - Acid extracted regenerated carbon-alum mixture - Battelle-
        Columbus process
FMCB  - Regenerated carbon-bentonite mixture - FMC process
FMCA  - Regenerated carbon-alum mixture - FMC process
AFMCA - Acid extracted regenerated carbon-alum mixture - FMC process
                                 -165-

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0.45 y membrane filters, and analyzed for organic carbon.
The data obtained are presented in Figures A-7,  A-8,  and
A-9.  These data indicate that capacity recovery lies some-
where between 90-100 percent.

A series of jar tests was run on sewage using virgin and
the various regenerated carbons.  Analyses performed on the
settled supernatants are presented in Table A-9.  The nutrient
results were predictable except for the apparent'removal of
NO" which cannot be explained.  Acid treatment of the re-
covered carbon-alum mixture produces a carbon which is
apparently as good as or better than the fresh product.

ALUM RECOVERY

An investigation was initiated to study the possibilities of
aluminum recovery from the regenerated carbon-alum mixture.
It is known that aluminum hydroxide goes through the conversion

           ,.. ,_„,  500°C   A, _   1000°C
           A1(OH)3  -v   Y-A1203    ^     a-A!203

The y-oxide readily dissolves in ^204 to reform Al ions
while the a-oxide is insoluble at reasonable acid levels.
Since carbon regeneration takes place below 1000°C, the
majority of the aluminum should be recoverable.   Two gram
samples of regenerated sludge were slurried and  acidified
over a range of pH values and the solution phase was then
analyzed for aluminum content colorimetrically.   This pro-
cedure was followed for both the first cycle and third cycle
BCL regenerated carbon-aluminum mixtures.  Results of these
experiments are summarized in Figures A-10 and A-ll.   Recovery
of approximately 86 percent of the aluminum at a pH of 1.75
was observed with the first cycle mixture.  Aluminum recovery
approached 100 percent for the third cycle case.  The acid
requirement was virtually identical in both cases.  At
this time, alum recovery appeared highly feasible.

Reuse of this recovered alum is discussed in the section on
the alum process optimization.

A similar line of investigation was pursued for  a Fe2(804)3
coagulant.  However, a red powder, believed to be Fe203  (which
should form at 200°C), formed in the thermal regeneration
step.  This iron oxide was very acid resistant and a good
dissolution to recover ferric ion could not be achieved at
reasonable acid levels.  It was concluded that the recovery
of Fe2S04, in this manner, was not feasible.

POLYELECTROLYTE SCREENING STUDY

Jar tests were run on a spectrum of commercial polyelectro-
lytes to identify those best suited for the operation.
                           -166-

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100
                                      VIRGIN  CARBON
                                      1st  CYCLE  ABCLA
                                      VIRGIN  CARBON
                                      2nd  CYCLE  ABCLA
                                      VIRGIN  CARBON
                                      3rd  CYCLE  ABCLA
                          REGENERATED  CARBON  DOSE
                          CORRECTED  FOR  ASH CONTENT
                 500            1000
                   CARBON DOSE (mg/£)
                               1500
   FIGURE A-7.
CAPACITY RECOVERY OF BATTELLE-COLUMBUS
   REGENERATED CARBON-ALUM PROCESS
                          -167-

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100
        I	1

       SEWAGE A

       SEWAGE B

       SEWAGE C
                                     VIRGIN CARBON
                                     1st CYCLE BCLB
                                     VIRGIN CARBON
                                     2nd CYCLE BCLB
                                     VIRGIN CARBON
                                     3rd CYCLE BCLB
                          REGENERATED CARBON DOSE
                          CORRECTED FOR ASH CONTENT
                 500
                   CARBON
   FIGURE A-8.
CAPACITY RECOVERY OF BATTELLE-COLUMBUS
 REGENERATED CARBON-BENTONITE PROCESS
                          -168-

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100
                                       VIRGIN  CARBON
                                       AFMCA
                                       FMCB
                            REGENERATED  CARBON  DOSE
                            CORRECTED  FOR  ASH CONTENT
                 500             1000
                   CARBON DOSE  (mg/4)
1500
FIGURE A-9.  CAPACITY RECOVERY OF FMC REGENERATED CARBONS
                          -169-

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                              TABLE A-9
              JAR TEST RESULTS WITH REGENERATED CARBONS
N03-N
(mg/1)
Influent
VC + Alum
VC +
BCLB
BCLB
FMCB
FMCB
ABCLA
ABCLA
VC
BCLB
bentonite
+ 150
+ 300
+ 150
+ 300
mg/1
mg/1
mg/1
mg/1
bentonite
bentonite
bentonite
bentonite
+ recovered alum
+ virgin
- Virgin
- Regener
alum

2
0
<0
<0
<0
<0
<0
<0
<0
.2
.22
.1
.1
.1
.1
.1
.1
.1
NH3-N
(mg/1)
31
28
27
26
27
27
26
26
26
PO,
(mg/1)
31
3
26
28
28
26
28
25
0
.2

.8
.8
.8
.8
.8
.4
.8
TOC
(mg/1)
41
9
11.
13.
16.
12.
13
8.
9.


5
5
5
5

5
5
carbon
ated carbon-bentonite mixture - Battelle-Columbus
        process
BCLA  - Regenerated carbon-alum mixture - Battelle-Columbus process
ABCLA - Acid treated regenerated carbon-alum mixture - Battelle-
        Columbus process
FMCB  - Regenerated carbon-bentonite mixture - FMC process
Carbon Dose = 1000 mg/1
                                -170-

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  60
  50
 '40
O
"30
  20
  10
  • 1st CYCLE

  O 3rd CYCLE

2 gm OF REGENERANT
MIXTURE WITH A CALCULATED AT
CONTENT OF 56.5 mg
                            pH
         FIGURE A-10.   EFFECT OF pH ON ALUMINUM RECOVERY


                              -171-

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10
                     T
                               « CYCLE  #1

                               O CYCLE  #2

                             2  gms  REGENERANT MIXTURE
I
                       I
                      I
           I
 6        12
VOLUME OF CONC.
18        24
 (mis x 1C)2)
                                                     30
      FIGURE A-ll.
         ACID REQUIREMENT VERSUS pH-BCL
               CARBON-ALUM MIXTURE
                           -172-

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                             TABLE A-10
        FLOCCULATION PERFORMANCE OF VARIOUS POLYELECTROLYTES
Polyelectrolyte
@ 10 mg/1
Nalco 600
Nalco 672
Magnifloc 837 A*
Magnifloc 905 K
Atlas 105-659
Atlas 300-400
Polyhall M-19
Purifloc N-17
Purifloc A-23
Purifloc C-23
Zetafloc WA
Performance in
Alum System
Negligible
Good
Good
Fair-Good
Good
Good
Fair
Fair
Very Good
Negligible
Poor
Performance in
Bentonite System
Negligible
Good
—
Good
Fair
Good
Fair
Fair
Negligible
Negligible
Negligible
*This is a commercial grade of Magnifloc 985 N
                                 -173-

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                             TABLE A-11
     EFFECT  OF  DOSE  ON  POLYELECTROLYTE PERFORMANCE - ALUM SYSTEM
                                  Performance






Dosage (mg/1)      1       2.1         5         7.5        10 '





Polyelectrolyte





Nalco 672         Poor  Poor-Fair    Good       Good       Good




Atlas 300-400     Fair    Good     Very Good  Very Good  Very Good




Purifloc A-23     Fair  Very Good  Very Good  Very Good  Very Good




Magnifloc 837 A   Poor    Fair       Fair       Good       Good
                                -174-

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Qualitative observations on the performance of these poly-
electrolytes appear  in Table A-10,  As a result of this
series, four brands  were selected for more extensive testing
in which doses were  varied from 1-10 mg/1.  Flocculating
characteristics observed in these tests are given in Table A-ll.

ALUM PROCESS OPTIMIZATION

It was decided to re-examine earlier results, which indicated
that a definite carbon contact time was required before alum
addition.  This point was critical, since the process would
be highly simplified if it was not necessary to separate the
reclaimed alum from  the carbon before reuse.  Jar tests were
devised whereby the  recovered alum was added simultaneously
with the carbon.  After a five minute contact time, caustic
was added to raise the pH and then, after an additional five
minutes, polyelectrolyte was added.  Flocculation proceeded
normally as long as  the caustic addition was regulated to
achieve the desired  effluent pH of approximately 7.  This indi-
cated that the recovered alum would not have to be separated
from the carbon as thought earlier.  Consequently, similar tests
were run on daily sewage samples for a period of two weeks in
conjunction with jar tests in which fresh alum was added simul-
taneously with the carbon.  The recovered alum solutions
exhibited good flocculation every time while several samples
in which fresh alum  was employed would not flocculate.  This
result suggested that the carbon could remove the interfering
substance if the solution was maintained in an acidified state
for the first few minutes of contact.  All subsequent observa-
tions reinforced this conclusion.

In order to further  investigate the feasibility of using re-
claimed alum, the bench scale system was set up with a chemical
addition line located downstream from the carbon contact tank
and pH probe located slightly further downstream.  Throughout
all of the runs, a lime slurry was pumped continuously in
sufficient quantity  to maintain the pH in the range of 6.5-7.0
at the downstream point.  In the initial run, a slurry of fresh
carbon and reclaimed alum was prepared and added in the same
manner as the carbon slurry in previous runs.  Doses were
1000 mg/1 C, 10 mg/1 Purifloc A-23 and 350 mg/1 alum.   A TOC
removal of 90 percent with a residual TOC of 9 mg/1 was observed.
Subsequent operation with a slurry of FMC regenerated carbon-
reclaimed alum resulted in an effluent with a residual TOC of
8.5 mg/1.

Additional bench scale experiments were conducted to study the
dose requirements of the polyelectrolytes which showed promise
in the beaker tests.  FMC regenerated carbon and reclaimed alum
were employed in these runs with the results given in^Table A-12,
Effluents of high quality were produced consistently in these
runs.  This process  employing regenerated carbon and reclaimed
                           -175-

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                        TABLE A-12
EFFECT OF POLYELECTROLYTE DOSE ON BENCH SCALE  PERFORMANCE
Influent
TOC Dose
(mg/1) Polyelectrolyte (mb/1)
129 Magnifloc 837-A 10
5
2.5
Atlas 300-400 5
2.5
Purifloc A-23 2.5
76 Nalco 672 2.5
5.0
10.0
Purifloc A-23 1.0
1.25
2.0
2.5
Atlas 300-400 1.25
2.5
Effluent
TOC
(mg/1)
16
14.5
14
12
10.5
10.5
0.0
0.0
4.0
0.0
0.0
2.5
0.0
0.0
0.0
TOC
Removal
(%)
87-7
88.9
89.2
90.8
91.9
91.9
>99
>99
95
>99
>99
97
>99
>99
>99
                            -176-

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alum with pH control proved to be highly reliable in the con-
tinuous flow laboratory system.

Based on these results, it was concluded that the Atlas 300-400
and Purifloc A-23 were the two polyelectrolytes best suited for
alum flocculation.

Data obtained in the carbon contact tests suggested that the
carbon dose could be reduced substantially below 1000 mg/1.
Subsequent jar tests confirmed that there was little difference
in effluent quality if the carbon dose was reduced from 1000
mg/1 to 600 mg/1.  Consequently, the bench scale system was run
at 600 mg/1 carbon.  Earlier jar tests also indicated that with
the Purifloc A-23, the alum dose could be reduced to as low as
150 mg/1.  The two new doses were checked simultaneously at a
Purifloc A-23 dose of 2.5 mg/1, with the results given below:

                              Alum  Influent  Effluent
                              Dose     TOC       TOC    Removal
                             (mg/1)  (mg/1)     (mg/1)      (%)

Inf. A-016 g/1 ABCLA carbon    150     105         3       97

Inf. B-016 g/1 Aqua Nuchar     200      88        11       88

Inf. A-016 ABCLA carbon        250     105         4       96

A small amount of carbon carryover was evident at the low alum
dose, but disappeared when the alum dose was increased to 200
mg/1.  It was concluded that satisfactory process performance
could be achieved with a carbon dose of 600 mg/1 and an alum
dose of 200 mg/1.  Further reduction in the carbon dose may
be possible with low TOC waste streams.

In order to investigate the effect of high solids and organic
loading on process performance, a special influent was pre-
pared by adding aged (60 days)  primary sludge to Richland raw
sewage.  The resulting mixture contained 2680 mg/1 total
solids and 1400 mg/1 TOC.  This waste was then treated in the
bench scale system with chemical doses at 600 mg/1 Aqua Nuchar
and 200 mg/1 alum.  Initially,  the system was operated at a
polyelectrolyte  (Purifloc A-23) dose of 10 mg/1 with a result-
ing residual TOC of 47 mg/1 or 97 percent TOC removal.  Effluent
TOC declined after startup and subsequent operation at a Puri-
floc A-23 dose of 2.5 mg/1 produced a product with a TOC resi-
dual of 17.5 mg/1, which represents 99 percent TOC removal.
Throughout the course of the run, effluent turbidities never
exceeded 1 JTU.  These results indicate that the treatment
process can easily handle waste streams with high solids
contents.
                           -177-

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       The system, at the conclusion of the laboratory studies,  had
       shown a high degree of  stability with little or no upset  at
       startup and rapid recovery  from pH disturbances.  Carbon
       carryover was unnoticeable,  turbidity consistently less than
       1 JTU, and TOG removals greater than 90 percent.
»U.S. GOVERNMENT PRINTING OFFICE 1973 514-153/199 1-3       ~178-

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  SELECTED WATER
  RESOURCES ABSTRACTS
  INPUT TRANSACTION FORM
                                        1. Report No.
                                                 2.
  4. Title Powdered Activated Carbon  Treatment of
        Combined and Municipal  Sewage
  7. Author(s) Shuckrow,  Alan J., Dawson,  Gaynor W.,  and
           Bonner,  William F.
  9. Organization Battelle
             Pacific Northwest Laboratories
             Richland, Washington    99352
                                    3. Accession No.

                                    W

                                    5. Report Date

                                    6- November, 1972
                                    8. Performing Organization
                                      Report No.

                                   10. Project No.
                                      11020  DSQ
                                   11. Contract/Grant No.
                                      14-12-519

                                   13. Type of Report and
                                      Period Covered
  12. Sponsoring Organization EPA, Office of  Research & Monitoring
  15. Supplementary Notes
                Environmental Protection Agency report
                number, EPA-R2-73-149, February 1973.
  16. Abstractive,  research program included laboratory  process development
   a unique physical-chemical wastewater treatment process followed by
design, construction, and field  demonstration of a 100,000 gpd  mobile
pilot plant.   In the treatment process, raw wastewater is contacted with
Dowdered carbon, coagulated with alum, settled with polyelectrolyte
addition and,  in some cases, passed through a tri-media filter.   The
 olids from the  clarifier, composed of raw sewage  solids, powdered carbon,
knd aluminum  hydroxide floe, are readily dewaterable to 20-25 percent
polids by direct centrifugation  with the powdered  carbon acting as a
 ubstantial aid  to dewatering.   The dewatered solids are passed through
a fluidized bed  furnace developed specifically for powdered carbon
regeneration.  Alum is recovered by acidifying the regenerated  carbon
slurry from the  furnace to a pH  of 2.   The recovered carbon and alum are
recycled as an acidified slurry  and added to the raw sewage with the
tiakeup carbon.   The program demonstrated the ability of tne treatment
srocess to consistently produce  high-quality effluent from raw  wastewater.
3owdered carbon  regeneration was highly successful on the pilot scale.
  ll capacity  recovery was achieved with less than two percent  carbon
Loss per regeneration cycle.  Alum recovery was also greater than ninety
percent.
 17a. Descriptors
   *Activated Carbon,  *Adsorption,  *Waste Water  Treatment
 17b. Identifiers

   *Combined Sewage
  17c. COWRR Field & Group
  18. Availability
19.  Security Class.
   (Report)

20.  Security Class.
   (Page)
  Abstractor A]_an  J.  ShuCkrOW
21. No. of
   Pages
  178
22. Price
                                               Send To:
                                               WATER RESOURCES SCIENTIFIC INFORMATION r-FM-r^
                                               U.S. DEPARTMENT OF THE INTERIOR      CENTER
                                               WASHINGTON. D. C. 20240
            institution Battelle , Pacific Northwest  LaboTlP
            	—-—••	torn
    102 (REV JUN E 1971 )

-------