S&A-TSB-22
  TECHNICAL  ASSISTANCE  PROJECT
    FORT   COLLINS  WASTEWATER
       TREATMENT FACILITY
    FORT   COLLINS,  COLORADO
    JANUARY    FEBRUARY,  1973
     TECHNICAL SUPPORT  BRANCH

SURVEILLANCE  AND  ANALYSIS DIVISION
    ENVIRONMENTAL  PROTECTION  AGENCY
             REGION  VIII

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                                          S&A/TSB - 22
       TECHNICAL ASSISTANCE PROJECT




FORT COLLINS WASTEWATER TREATMENT FACILITY





         FORT COLLINS, COLORADO




        JANUARY - FEBRUARY, 1973
        TECHNICAL SUPPORT BRANCH




   SURVEILLANCE AND ANALYSIS DIVISION




  U. S. ENVIRONMENTAL PROTECTION AGENCY




               REGION VIII







                MAY, 1973

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                         TABLE OF CONTENTS









  Section                                              Page No.




  I.   Introduction^	    1




 II.   Description of Plant	    1




III.   Summary of Assistance Project	    4




      A.  Control Testing	    4




      B.  Process Modifications	    5




      C.  Performance Results	   15




IV.   Summary and Conclusions	   21




 V.   Recommendations	   24

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                      LIST OF FIGURES







Figure                                            Page No.




1.   Plant Flow Schematic	     2




2.   Effluent BOT)^ vs Time	     17




3.   Effluent TSS vs Time	     18




4.   Percent Reduction of BOD,, vs Time	     20

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 I.  Introduction




      On October 25, 1972, personnel from the Environmental Protection Agency,




 Region VIII, and from the Colorado State Department of Health conducted an




 operation and maintenance survey of the Fort Collins Wastewater Treatment




 Plant #2 (activated sludge plant).  The data collected during this study showed




• that the Fort Collins plant generally was producing a good quality effluent.




 However, the data also indicated that cycles of good quality effluent and poorer




 quality effluent were occurring.  In an effort to produce a consistently high




 quality effluent, a technical assistance project was initiated at the Fort




 Collins facility on January 15, 1973.




      The purpose of this report is to document the results from the technical




 assistance project.  The operational controls initiated during the project as




 well as design limitations observed are outlined in the report.  The results




 achieved in producing a consistently high quality effluent are also discussed.




      It is noted that Fort Collins also operates and maintains a trickling




 filter wastewater treatment facility.  No assistance was provided concerning




 this plant.




 II.  Description of Plant




      The Fort Collins Plant #2 is an activated sludge facility which treats




 primarily domestic sewage from the south portion of the City.  The daily average




 flow in 1972 was about 20,817 cu. in/day (5.5 MGD) during the summer (high flow




 due to infiltration)  and 15,112 cu. m/day (3.9 MGD) during the winter.




      Figure 1 depicts a schematic diagram of the various plant units.  Flow




 enters the plant by gravity and is pumped to the primary clarifiers.  Raw




 sewage may also be pumped, if required, directly to the distribution channel




 between the two aeration basins.  Effluent from the primary clarifiers enters




 the distribution channel between the two aeration basins and is directed to




 the basins by opening or closing the appropriate sluice gates.  Sluice gates

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To Cache La Powdre River
     Sludge and^/
     Grease
                                               mary      V        '	'
                                               rifier     ^West Aeration Basin
                                                                                                       FIGURE 1

                                                                                             TECHNICAL ASSISTANCE PROJECT
                                                                                                PORT COLLINS WASTEWATER
                                                                                                  TREATMENT FACILITY
                                                                                                FORT COLLINS, COLORADO

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are located at the head end and half way down each aeration basin.  Flow from




the primary clarifiers can by-pass the aeration basins directly to the secondary




clarifiers or to the chlorine contact basin.  This by-passing may be accomplished




by opening or closing a sluice gate located at the end of the aeration basin




distribution channel.




     Mixed liquor from each aeration basin is directed to a collection box




located at the end of the two basins.  Flow from the collection box is distributed




to the final clarifiers through mud valves.




     Sludge is collected in the secondary clarifiers by suction type scraper




mechanisms and is returned through a common header to the aeration basins by




three variable speed centrifugal pumps.  These pumps may be used and adjusted




independently.  Return sludge may be added to the aeration basins through ports




at the head end of the basins or through ports located halfway down the basins.




Return sludge flow is measured by an inline venturi meter.




     Excess activated sludge is wasted to the raw sewage wet well and then




pumped to the primary clarifiers.  Prior to assistance, excess activated




sludge was wasted by lowering a telescoping valve located on the return sludge




line.  During assistance this valve was plugged and sludge was wasted by




opening a two-inch gate valve located on a two-inch pipe which was welded




into the telescoping valve.  The waste sludge flow rate varied with changes in




the return sludge flow.  Therefore, it was necessary to determine the wasting




rate at various return sludge flow rates.




     Effluent from the secondary clarifier is directed to a chlorination basin




and is discharged to the Cache-La Poudre River.




     Sludge and grease from the primary clarifiers. are pumped to anaerobic




digesters which are being operated in series (i.e., primary, secondary




digesters).

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Ill.  Summary of Assistance Project




          It was felt initially that the project at Fort Collins would be




directed at initiating control testing procedures to enable the operators to




"fine tune" the facility and eliminate the fluctuations in effluent quality.




It was determined, however, that some modifications were required to the




existing facilities to achieve desired operational results and flexibility.




Some of the desired modifications could not be made during the assistance pro-




ject and these changes will be discussed in the recommendations.




     A.  Control Testing




          A series of control tests were initiated at the Fort Collins facility




to enable the operators to closely monitor the processes and to indicate when




process controls needed to be changed (i.e., adjustment of return sludge flow




rates, adjustment of the quantity of activated sludge to be wasted, adjust-




ment of dissolved oxygen concentrations, etc.).  Several of the control tests




initiated were used by plant personnel before the assistance project.  These




tests were modified slightly and incorporated into a routine testing procedure.




          The control tests initiated were dissolved oxygen determinations,




centrifuge tests, turbidity, settleability tests, and sludge blanket depth




determinations.  These tests were conducted four times per day, seven days per




week.




          Dissolved oxygen (D.O.) tests were used to monitor the availability




of D.O. in the aeration basins.  The most critical points for the availability




of D.O. were determined by taking measurements throughout the length of the




basins.




          Centrifuge tests were used to determine variations in solids concen-




trations throughout the day and from day to day.  Tests were conducted on samples




of mixed liquor taken at the discharge end of each aeration basin and on samples

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of return sludge.  The centrifuge test values are expressed in percent solids




by.volume.  Although it is not necessary for control, a correlation between




percent solids by volume and solids by weight was made.  The results of this




correlation indicated that during the project one percent solids by volume was




approximately equal to 670 mg/1 by weight.  This correlation will vary as the




characteristics of the sludge varies.  For this report all solids concentrations




by weight were determined by using the correlation of one percent by volume equal




to 670 mg/1 by weight.




     Turbidity tests were performed on samples of the effluent from one of the




final clarifiers.  Test results were used to minotor the performance of the




activated sludge process prior to obtaining ,a BODj result.




     Settleability tests were conducted on samples of the mixed liquor collected




at the discharge end of the aeration basins.  Settleability tests were used to




monitor and observe sludge settling characteristics.




     Sludge blanket depth determinations were made on the final clarifiers.




Results were used to monitor changes in the depth of the blanket and to determine




the amount of sludge that was accumulating in the final clarifier.  It is noted




that the blanket depth determinations and wasting control procedures were begun




after the initial EPA inspection in October, 1972.  The effect of using this




portion of the control testing procedures will be shown when effluent quality




is analyzed.




     Data obtained from the various control tests were used to perform calcula-




tions and develop various graphs.  The results of the calculations and the




trends from the graphs were used to interpret plant performance and control




plant operations.




     B.  Process Modifications




          During the assistance project, various problems were encountered that




inhibited plant operation and flexibility.  In most cases, these problems were




corrected by plant personnel.  In fact, plant personnel are to be commended

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for their efforts in utilizing available material to satisfactorily complete




the required physical modifications within a short period of time.  Other




modifications that could improve plant performance could not be completed




during the assistance project.  These modifications will be presented and dis-




cussed in the report for future considerations at the Fort Collins plant.




          1.  Physical Modifications




               The first change made at the Fort Collins Plant #2 involved the




method of returning activated sludge and wasting excess activated sludge.  Prior




to assistance the return sludge flow was divided as equally as possible between




the four return sludge ports located in the aeration basins (See Figure 1).




To eliminate any possibility of sludge "short circuiting" through the aeration




basins it was decided to return the activated sludge through the two ports




located at the head end of each aeration basin.  When this was attempted, the




increased pressure required to force the return sludge to the head end of the




aeration basins was sufficient to force solids out of the telescoping valve used




for wasting excess activated sludge and thus solids were wasted unintentionally.




Therefore, the telescoping valve was plugged, and an alternative method of




wasting was accomplished by welding a valved two inch pipe into the telescoping




valve.  This method of wasting allowed for smaller amounts of excess activated




sludge to be removed from the system over longer periods of time.




               Operational problems were encountered in trying to adjust return




sludge flow rates to achieve optimum solids removal with a minimum amount of




water contained in the return sludge.  The control tests indicated that dis-




crepancies existed in the laboratory data and the performance of the facility.




An investigation led to the discovery of leaking seals located around the




return sludge center well of each of the suction type secondary clarifiers.




The effect of the leaky seals was to allow mixed liquor to dilute the return




sludge flow.  In fact, a solids balance conducted around the final clarifier




indicated that approximately 40 percent of the return sludge flow was comprised

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of mixed liquor.  Excessively high return rates were required to compensate




for the dilute return sludge and to maintain a desired solids concentration in




the aeration basins.  It is also felt that a portion of the cycling problem




that Fort Collins experienced with effluent quality can be attributed to the




leaking seals.  The leak inhibited proper adjustment of return sludge flow




rates and thus allowed the plant to operate somewhat at its own will.




               In an effort to conserve time, the seals on both clarifiers were




replaced in a one-day period.  Although this virtually eliminated the leaking




problem, it also served to remove all the solids contained in both final




clarifiers from the system.  (They were wasted to the primary clarifiers.)




This solids loss had a terrific impact on the assistance project as was deter-




mined through operational difficulties encountered after the seals were fixed.




This aspect of the assistance project will be discussed later in the report.




It is recommended that the seals be routinely checked at least once a year




and replaced when necessary.  It is also recommended that the -replacement




process be designed to eliminate excessive losses of sludge from the activated




sludge system.




               Prior to assistance, personnel at the Fort Collins wastewater




treatment plant were operating the mud valves used to direct the flow to the




final clarifiers so that the flow or mixed liquor would "back up" in the




aeration basins.  This operation served a dual purpose of equalizing a small




amount of the incoming sewage flow and also increased the liquid depth in the




aeration tanks allowing the fixed surface mechanical aerators to supply




additional oxygen to the mixed liquor.  Two problems were encountered with




this kind of operation.




               The first problem was one of providing a consistently adequate




supply of dissolved oxygen.  After several other methods had been tried, a




solution to controlling the dissolved oxygen concentration was achieved by




raising the adjustable weir on the effluent from the aeration basins.  These

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weirs had not been adjusted for several years and had rusted tight in the




lowered positions.  Raising the weirs allowed the water level in the basins




to increase and thus enabled the fixed mechanical aerators to supply additional




oxygen.  The advantage of this arrangement was that water did not have to be




"backed up" in the aeration tanks daily to ensure an adequate supply of oxygen.




During the process of raising the effluent weirs on the aeration basins it




was noticed that the rubber seals along the bottom of the weirs was leaking.




In fact, the leak in the west aeration basin was so severe that a hydraulic




imbalance was created between the aeration basins and it became difficult to




achieve equal mixed liquor concentrations between the two basins.  To compen-




sate for this leak, a portion of the effluent weir on the west basin was




blocked off and more equal mixed liquor concentrations were obtained.  It is




recommended that the more permanent solution to the problem would be replacing




the rubber seals along the adjustable weir.  It is also recommended that these




seals be routinely checked at least once a year and that care be taken when




replacing the seals to avoid excessive losses of sludge from the activated




sludge system.




               The second problem encountered by daily adjusting the mud valves




to the final clarifiers was one of flow distribution.  Many times the quantity




of sludge in one clarifier would greatly exceed the quantity in the other.




Since mud valves are not good valves for flow control, it was felt that if both




valves could be left wide open that equal flow and thus sludge distribution




would result.  This proved not to be the case; however, since the collection




box where the mixed liquor is directed to the final clarifiers was not symmetri-




cal.  The turbulence and non-symmetrical arrangement of this collection box




caused flow variations between the final clarifiers to occur.  A wooden baffle




was placed in the collection box to eliminate a portion of the turbulence.




This resulted in a more uniform flow distribution to the final clarifiers.

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               The final clarifiers at Fort Collins are equipped with a




suction-type scraper mechanism.  An operational problem was encountered in




trying to "draw" a uniformly thick concentration from each of the eight re-




moval ports.  Adjustments were made to try to balance the return sludge con-




centration from each port.  It is recommended that these ports be monitored




routinely to insure a uniform sludge concentration in the return sludge flow.




          2.  Operational Modifications




               Initially, it was felt that the lack of fine tuning was causing




the cycling effect in the effluent quality at the Fort Collins #2 plant.




However, it was determined that this was not the problem.  The major operational




problem at the Fort Collins plant is one of developing and maintaining a




mature good settling sludge.  After discussing past difficulties encountered




by present and previous operators, it became apparent that this problem has




plagued the plant since it began operation.




               Developing and maintaining a mature good settling sludge at




Fort Collins requires that a sufficient mass of sludge be held in the system




to insure favorable food to micro-organism ratios consistent with the




physical facilities provided.  When both seals in the final clarifiers were




replaced, a large portion of the solids that the operators had accumulated




in the system were removed.  The result of this loss of solids was that a




poor settling sludge developed in the system.  The first attempt at improving




sludge settleability was to simply stop wasting and let the sludge mass




increase to a desired level.  This proved to be difficult since solids would




readily "bulk" from the final clarifiers and not allow a substantial increase




in sludge mass in the system.  This has been a continual problem at the




Fort Collins plant in the past.  The relationship of the size of the clarifiers




and aerators at the facility is such that increasing solids to a desired level




is hindered because bulking in the final clarifiers limits an increase in sludge

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mass by "automatically" wasting solids from the system.  First glance at this




problem indicates that additional clarifiers are needed to eliminate the bulk-




ing.  Although this may provide a solution, it is not felt that this is the




most desirable approach.




               Aeration basin detention time is a limiting factor in allowing




the development of a good settling sludge at the Fort Collins facility.  Normal




aeration basin detention times are from 6 to 8 hours for conventional activated




sludge systems.   Based on daily average flows aeration basin detention times




at Fort Collins  range from a high of 5.7 hours during winter months (Flow =




14,383 cu. m/day (3.8 MGD))to a low of 3.9 hours during summer months when




infiltration occurs (Flow = 20,817 cu. m/day (5.5 MGD)).  Although the Fort




Collins plant is designed to operate as a conventional type of facility the




aeration basin detention times are minimal.  This problem is accentuated when




a poor settling  sludge exists in the system.  Poor settling sludges require




high return sludge flow rates to maintain a desirable solids concentration in




aeration basins.  The effect of the high return rates is that it cycles the




sludge quickly through the aeration basin.  For example, the effective sewage




detention time is equivalent to the volume of the aeration basins divid.ed by




the incoming flow while the effective sludge detention time in the aerator is




equivalent to the volume of the aeration basins divided by incoming flow plus




the return sludge flow.  This factor becomes increasingly significant when




trying to develop a mature good settling sludge.




               To develop a good settling sludge requires that the sludge be




in the environment of the aerator in sufficient quantity so that desirable




food to micro-organisms ratios are achieved.  Therefore, it was decided to




try to operate the Fort Collins facility in the contact stabilization mode.




All of the return sludge flow was returned to the head end of the aeration




basins while the incoming sewage was introduced at the inlet gates located




half way down the aeration basins.  Supposedly, the head end of the aeration





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basins should have contained sludge at a concentration approximately that of




the return sludge flow and thereby should have increased the mass of sludge in




the aeration basins.  However, due to the effective mixing provided by the




surface mechanical aerators, no differentation of solids concentration could




be detected in the aeration basins.  The method of using contact stabilization




to provide adequate sludge detention time in the aeration basins would be




desirable especially during the summer months when high infiltration occurs




and aeration basin detention times are at a minimum.  A suggested arrangement




would be to use one aeration basin as a reaeration tank and one as a contact




tank.  A few minor modifications would give the operators the contact stabili-




zation flexibility.




               Along these same lines an approach to increase the mass of




sludge at the Fort Collins plant was devised.  Since it was difficult to




increase solids without severe bulking, it was decided to use one of the




aeration basins to store solids until a desired mass was accumulated.  This




was accomplished by loading only one aeration basin with incoming sewage and




putting only a portion of the return sludge flow in the other basin.  This




allowed an accumulation of solids at a higher concentration in the aeration




basin not receiving any sewage flow.  When the desired mass of solids had




been accumulated in the system, the plant was switched back to the conventional




mode of operation (i.e., all sewage and return sludge introduced at the head




end of the aeration basins).  High mixed liquor concentrations (approximately




equal to 3000 mg/1)  were achieved in both aeration basins.  The poor settling




solids were kept in the system by minimizing bulking.  The procedure used to




minimize bulking was to by-pass primary effluent directly to the final clari-




fiers and thus decrease the solids loading on the secondary clarifiers.  This




method of operation was carried on about a week to give the sludge a chance to




develop better settling characteristics.  As the sludge began settling better,




less and less primary effluent had to be by-passed to the secondaries and




finally all the flow was handled through the aeration basins.




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               In summary, the aeration basins and final clarifiers at Fort




Collins are sized so that difficulties are encountered in trying to develop




and maintain a good settling sludge.  The major factor influencing these




difficulties is the minimal size of the aeration basins.  When low solids




concentrations occur, such as during start-up or as a result of breakdowns




or maintenance, it is recommended that the procedure used during assistance




(i.e., building solids in one aeration basin and storing them in the other) be




used to aid in rapid development of a good settling sludge.




               Another major operational problem at the Fort Collins plant is




the limited time during the day the plant is operated.  Due to the relatively




small aeration basins it becomes necessary to continually readjust return




sludge flow rates as the flow changes.  For example, in extended aeration




activated sludge plants (aeration basin detention time = 24 hours) the incoming




flow has little impact on the contents of the large aeration tank and as a




result, return adjustments, although necessary, are not as critical.  The




smaller the aeration basin becomes  (i.e., shorter detention times) the more




sensitive the mixed liquor concentration is to the incoming flow.  Since the




Fort Collins plant has only eight hours a day operation all adjustments to




return rates must be accomplished in an eight-hour period.  This proved to be




unsatisfactory during the assistance project ,and plant personnel were requested




to come in "after hours" to make adjustments in return sludge flow rates.




However, the flow does not significantly change until 2:00 a.m. in the morning,




and this was too late to expect the operators to stay on the job.  The result




of not adjusting return sludge flow rates especially in a plant with short




aeration basin detention times is that a lower inventory of solids must be




carried to avoid bulking problems.  The lower solids inventory and the lack




of return adjustments to maintain the highest mixed liquor concentration




possible, results in a poorer quality effluent than could be achieved if




return adjustments were made.  It is recommended that twenty-four-hour





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operation be provided at the Fort Collins facility so that optimum performance




can be achieved.




          3.  Future Modifications




               Although numerous operational and physical modifications were




made at the Fort Collins plant several areas that pose operational problems




still exist.  Perhaps the most significant area of difficulty encountered at




the Fort Collins plant was the relationship between the volume of the aerators




and the clarifiers.  The effect of this imbalance in volumes can be pointed




out by first comparing two variations of the activated sludge process (i.e.,




high rate processes versus conventional processes).  High rate activated sludge




processes are characterized by relatively small aeration basins and large final




clarifiers.  Settling characteristics associated with the process are generally




considered to be relatively poor.  Conventional activated sludge processes




generally exhibit better settling characteristics and are characterized by




larger aeration basins and smaller clarifiers in relation to a high rate




process.  At Fort Collins the relatively short detention times in the aeration




basins result in the process tending toward the high rate activated sludge




variation.  As a result, the clarifiers appear to be unsatisfactory any time




the system gets out of balance.  Although an additional clarifier may provide




satisfactory performance, a better approach would be to provide additional




aeration capacity.  This would enable the process to tend more toward the con-




ventional activated sludge process and its associated better settling character-




istics.  The result would be to provide a more easily controllable plant




capable of producing a higher effluent quality.




               Another modification that would aid the operators in control-




ling the present facility would be to provide them with the flexibility to




operate one aeration basin as a reaeration tank and the other as a contact




tank.  This modification would allow plant personnel to maintain a high




inventory of sludge during the summer months when infiltration rates increase





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significantly.  During the summer months in the past, difficulties have been




encountered in maintaining an adequate amount of sludge due to solids losses




in the effluent from the final clarifiers.




     Another area of operational difficulty was encountered in trying to




adjust and maintain low return sludge flow rates.  Low rates were accomplished




by partially closing the plug valves provided on the discharge side of the




centrifugal return sludge pumps.  This proved unsatisfactory because during




the night the valves would become plugged with debris and significantly reduce




the desired return flow rates.  This problem could be reduced if twenty-four




hour operation were provided.  Also, at low return sludge rates precise flow




measurement was difficult.  It is suggested that additional flow meters that




provide more precise flow readings at low flows  (i.e., less than 63.1 I/sec




(1000 gpm))  be installed.  Consideration should also be given to providing




a smaller return sludge pump so that valving with the associated plugging




problems could be minimized.




     Waste sludge flow control and measurement at the Fort Collins plant lacks




the flexibility that the operator needs to maintain close control over his




process.  Waste sludge flow rates are difficult to determine and change




constantly as the return sludge flow, rate is adjusted.  A more desirable and




controllable approach would be to provide a wasting system that is separate




from the return sludge system and one where wasting rates could be adjusted




to a desired level and measured.




     Two other modifications that would assist plant personnel in providing a




consistently high quality effluent would be to provide the flexibility to use




one or both of the primary clarifiers as flow equalization basins and to provide




the capability to add polymers or chemicals to the aeration basin effluent to




aid settling in the final clarifiers.




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               Flow equalization could be accomplished by providing a method




for the primary clarifiers to drain to the influent wet well during the night.




The result of this modification would be to lessen the impact of peak daily




flows on the mixed liquor solids concentration in the present aeration basins.




Also, the solids loading rate on the final clarifiers would be lessened by




decreasing the magnitude of peak flows.




               The ability to add polymers and chemicals to the mixed liquor




to aid settling would allow the operators to minimize solids losses in the




effluent during period of imbalance (i.e., breakdowns, shutdowns for main-




tenance, periods when poor settling sludge exists, etc.)




     C.  Performance Results




          The primary objective of the technical assistance project at Fort




Collins was to produce a consistently high quality effluent.  To demonstrate




the "cycling" effect on plant effluent quality, plant data was analyzed for




4-1/2 months prior to the initiation of the assistance project.  A period of




4-1/2 months after initiation of the assistance project was also analyzed to




show the results of assistance.  Data analyzed included the biochemical




oxygen demand (BOD5) of the plant influent, final clarifier effluent, and




chlorine contact tank effluent (i.e., plant effluent) and the total suspended




solids (TSS)  of the chlorine contact tank effluent.  The samples for these




analyses were collected three times each day and were composited.  No attempt




was made to composite samples proportional to flow.  The laboratory analyses




were performed the following day.




          During the assistance project, plant operators spent a considerable




amount of time repairing plant deficiencies noted during assistance and




learning and using the techniques initiated to control plant operation.  Due




to this increased demand on their time, the TSS results are incomplete during




the course of the assistance project.







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          Figure 2 shows the 7-day moving average BOD- concentration of the




final clarifier effluent and chlorine contact tank effluent.   Figure 3 shows the




7-day moving average TSS concentration of the chlorine contact tank effluent.




Data is shown for the period of September, 1972, through May,  1973.  These




figures show the cycling of effluent quality that occurred prior to the




assistance project (before January 15, 1973).  The BODg concentration of the




final clarifier effluent varied from about 55 mg/1 to about 13 mg/1 and the




BOD,- concentration of the chlorine contact tank effluent (plant effluent)  varied




from about 45 mg/1 to about 10 mg/1.  The plant effluent TSS  concentration




varied from about 63 mg/1 to about 15 mg/1.  The fluctuations in effluent quality




are in part a result of many of the deficiencies that existed in the facility




prior to technical assistance (i.e., leaky seals, inadequate  flow splitting,




small aerators, return sludge flow control, etc.)




          It should be noted that a portion of the operational controls used




during the formal assistance project were initiated approximately one month




prior to beginning the project.  (Shown on Figures 2 and 3).   After initiation




of these controls plant effluent BOD^ concentrations were achieved below 20 mg/1




and are comparable to BOD5 concentration values achieved after completion of




the assistance project.  Plant effluent TSS, however, was between 20 and 30 mg/1




during this one month period, much higher than TSS values achieved after




completion of the assistance project.  Apparently, changes in plant operation




as a result of the assistance project provided conditions for better solids




capture and lower TSS values.




          During assistance plant effluent quality was not satisfactory due to




operational problems encountered as a result of the many changes.  After these




operational problems were solved, however, plant effluent BOD5 and TSS values




were never greater than 20 mg/1 (i.e., the 1975 Colorado Effluent Standard).




The final clarifier effluent BOD  value did exceed 20 mg/1 for a short period




of time during the first of May.  These higher BOD- values can be attributed





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 50,
40
30
20
10
                                                                                                                                 TECHNICAL  ASSISTANCE PROJECT
                                                                                                                                   FORT COLLINS  WASTE WATER
                                                                                                                                      TREATMENT  FACILITY
                                                                                                                                    FORT COLLINS,  COLORADO
                                                                                            EFFLUENT BOD
                                                                                                 VS.
                                                                                                TIME
                                                                                                                                 7-DAY MOVING  AVERAGE
                                                                                                                                 BEFORE CHLORINATION
                                                           7-DAY MOVING
                                                           AVERAGE AFTER
                                                           CHLORINATION
         10    20    30
            SEPTEMBER
                             OCTOBER
                                        30
10    20
NOVEMBER
                                                           30
                                                                  DECEMBER
10    20
  JANUARY
10    20
 FEBRUARY
10     20
 APRIL
                                                                                                                                                      30
 10
MAY
20

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60
          FIGURE  3

TECHNICAL ASSISTANCE PROJECT

  FORT COLLINS WASTE WATER
     TREATMENT FACILITY
   FORT COLLINS,  COLORADO

  EFFLUENT SUSPENDED SOLIDS
             VS.
            TIME
                                                                              TIME

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to higher plant flows  (due to infiltration) and the associated problems with




the relatively short aeration basin detention times and inadequate return




sludge flow control  (due to limited plant staffing).  These problems were




partially overcome by the end of the month of May.  The fluctuations in plant




effluent quality (i.e., periodic high BOD- and TSS values) can be expected to




continue as long as the problems with the short aerator basin detention time




and inadequate plant staffing continue.  The length of time and number of




times the plant experiences these high BOD5 and TSS values should be reduced




due to the operational controls provided at the plant as a result of the




assistance project.




          Figure 4 shows the percent removal of BOD^ through the entire plant




(i.e., plant influent through chlorinated effluent) and through the final




clarifier effluent (i.e., plant influent through final clarifier effluent).




The total plant BOD  removal percentage was always greater than 90% after




assistance.  The difference in the BOD- removal .percentages and BOD,, concen-




trations in the chlorinated effluent from those shown for the final clarifier




effluent may be attributed to reductions in the BOD5 due to chlorination




and possible chlorine interference with the BOD_ test (chlorinated effluent




samples are not dechlorinated).  The differences between these results are




not always consistent and can be expected to vary as the plant performance




varies.  It is felt that the most accurate measure of the activated sludge




performance is provided by final clarifier effluent sample analysis.  To




accurately measure the activated sludge performance it is suggested that final




clarifier effluent BOD,- analysis be continued.




          Results of the data analysis shown in this portion of the report




indicate that a consistently high quality effluent was developed and main-




tained for approximately 2-1/2 months.  However, the more important results




are that the present plant operators were provided the means to recover from




poor effluent quality in a minimum amount of time.





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100
                                                                                                                                                                AiA
                I   AVERAGE  AFTER
                 4  CHLORINATION
            7-DAY MOVING
            AVERAGE BEFORE
            CHLORINATION
                                                                                                                          TECHNICAL ASSISTANCE PROJECT
                                                                                                                            FORT COLLINS WASTE WATER
                                                                                                                               TREATMENT FACILITY
                                                                                                                             FORT COLLINS, COLORADO
 60
          10    20    30
            SEPTEMBER
10    20    30
   OCTOBER
10    20    30
  NOVEMBER
10    20    30
  DECEMBER

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IV. Summary and Conclusions




     Data collected during an operation and maintenance survey of the Fort




Collins Wastewater Treatment Plant #2 indicated that cycles of good quality




effluent and poorer quality effluent were occurring.  A technical assistance




project was initiated by personnel from Region VIII of the U.  S. Environmental




Protection Agency on January 15, 1973, in an effort to produce a consistently




high quality effluent from the Fort Collins facility.




     A series of control tests and daily calculations were initiated at the




Fort Collins facility to enable the operators to closely monitor the processes




and to indicate when process controls needed to be changed.  It is recommended




that these control tests and calculations continue to be used to guide the




operators in maintaining good operational control.




     Initially, it was felt that the assistance project would be directed at




"fine tuning" the facility.  However, both physical and operational modifi-




cations were required to achieve desired results and flexibility.




     The series of important physical modifications made to the Fort




Collins facility are summarized below:




          1.  A modification was made to the location that the return sludge




was introduced to the aeration basins (i.e., all return sludge was introduced




at the head end of each basin).




          2.  The method of wasting excess activated sludge was changed to




allow smaller amounts of sludge to be wasted over longer periods of time.




          3.  Leaky seals were discovered and replaced in the center well of




the final clarifiers.  Routine maintenance inspections and replacement of




these seals is required in the future.




          4.  The adjustable effluent weirs on the aeration basin were placed




into service to provide a means of flexible dissolved oxygen control.  The




seals adjacent to these weirs were observed to be leaking and replacement




is recommended in the near future.




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          5.  A wooden baffle was placed in the collection box at the end of




the aeration basins to eliminate excessive turbulence and allow a more equal




distribution of flow to the final clarifiers.




          6.  Modifications and adjustments were made to the return sludge




ports in the final clarifiers to achieve removal of a uniformly thick return




sludge.




     Operational modifications were developed at the Fort Collins plant to




minimize the time required to grow and maintain a good activated sludge.  A




large amount of sludge was initially wasted from the Fort Collins plant when




the leaky seals in the final clarifiers were replaced.  The poor settling




sludge that developed after this solids loss and the problems encountered in




trying to increase the sludge mass indicated that one of the main operational




problems at the Fort Collins facility was developing and maintaining a mature




good settling sludge.  This fact was supported by prior difficulties that




plant personnel had experienced in 'maintaining consistent control over the




facility.  A method to increase the sludge mass to a quantity that would




encourage the development of a good settling sludge was achieved after several




different attempts.  The method involved using one of the aeration basins to




"store" activated sludge solids while the other aerator was used to treat the




incoming sewage and grow solids.  After a desired mass of solids were




obtained, they were dispersed throughout the system and held until a good




sludge had a chance to develop.  This method can be used in the future to




rapidly  develop a desired sludge.




     Other operational modifications used during the project were to initiate




"after hours" adjustment of process controls.  Future operation of the facility




should include greater than eight hour a day operation or effluent quality will,




of necessity, be less than optimum.  Twenty-four hours a day operation is




recommended.




     Other modifications that would improve plant performance at Fort Collins





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could not be completed during the assistance project.  These Modifications are




summarized below:




          1.  It is suggested that consideration be given to adding additional




aeration capacity at the Fort Collins plant to provide a more easily controll-




able facility capable of producing a higher quality effluent.




          2.  The capability of operating one aeration basin as a reaeration




tank and one basin as a contact tank (i.e., similar to the contact stabiliza-




tion variation of the activated sludge process) should be provided at the




Fort Collins facility.




          3.  Difficulty was encountered in adjusting and maintaining low




return sludge flow rates.  Consideration should be given to providing a




smaller pump and metering equipment that would provide precise measurement




and control at low return rates.




          4.  Inadequate flow control and measurement still exist on the




waste sludge flow system despite modifications that were made.  It is




suggested that an independent wasting system be developed and variable flow




control and metering be provided.




          5.  The capability of using one or both of the primary clarifiers




as flow equalization basins would provide the operator with flexibility to




maintain a higher solids mass in his system especially during summer months




when infiltration occurs.




          6.  The capability to add polymers and chemicals to aid settling




would allow the operators to minimize solids loss during periods of im-




balance.




     The primary objective of the assistance project at Fort Collins was




to produce a consistently high quality plant effluent.  As a result of the




project the cycling effect was reduced substantially.  Periodic effluent




quality fluctuation can be expected, however, due to problems with the




short aeration basin detention time and inadequate plant staffing.





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     Plant effluent BOD  concentrations had been reduced during the month




prior to assistance to below 20 mg/1.  However, effluent TSS concentrations




were between 20 to 30 mg/1.  A portion of the operational controls used




during assistance had been initiated during this time.  After assistance,




the seven-day moving average values of BOD,, and TSS concentrations in the




plant effluent were below 20 mg/1.  Apparently, changes in plant operation




as a result of the assistance project provided conditions for better solids




capture and lower TSS values.  Seven-day moving averages of BOD,, removal




percentages for the plant were consistently greater than 90% after completion




of the assistance project.




V.  Recommendations




     The following recommendations are made:




          1.  Control tests and calculations initiated during the assistance




project should be continued.




          2.  The rubber seals in the center well of the final clarifiers and




adjacent to the effluent weirs on the aeration basins should be inspected




routinely and replaced when necessary.




          3.  The operational mode used during assistance to develop a good




settling sludge should be used when required in the future to minimize




periods of poor effluent quality.




          4.  Twenty-four hour a day operation should be provided at the




treatment facility.




          5.  Additional aeration capacity should be considered.




          6.  Flexibility to operate in the "contact stabilization" mode




should be provided.




          7.  Modifications to provide better return sludge flow control and




measurement at low rates should be provided.




          8.  Modifications to provide better waste sludge flow control and




measurement should be provided.  Consideration should also be given to separa-





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tion of the wasting and return sludge flow systems.




          9.  Flexibility to use the primary clarifiers as flow equalization




basins should be provided.




         10.  Flexibility to add polymers and chemicals to the mixed liquor




to aid settling should be provided.
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