S&A-TSB-23
      TECHNICAL ASSISTANCE  PROJECT
UPPER  EAGLE  VALLEY   SANITATION  DISTRICT
     WASTEWATER  TREATMENT  FACILITY
              AVON,   COLORADO
            MARCH  -   APRIL,  1973
                ' ;'",^t^-- - ••

          I
         TECHNICAL  SUPPORT  BRANCH
    SURVEILLANCE AND ANALYSIS  DIVISION

    S. ENVIRONMENTAL  PROTECTION  AGENCY
                 REGION  VIII

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     TECHNICAL ASSISTANCE PROJECT





UPPER EAGLE VALLEY SANITATION DISTRICT





     WASTEWATER TREATMENT FACILITY




            AVON, COLORADO





           MARCH-APRIL, 1973
       TECHNICAL SUPPORT BRANCH





  SURVEILLANCE AND ANALYSIS DIVISION





 U.S. ENVIRONMENTAL PROTECTION AGENCY





              REGION VIII





              JUNE, 1973

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                              TABLE OF CONTENTS







      SECTION                                                   PAGE NUMBER








  I.   INTRODUCTION	     ]_





 II.   DESCRIPTION OF PLANT	     1





      A.   BACKGROUND	     1





      B.   PLANT FACILITIES	     2





III.   SUMMARY OF ASSISTANCE PROJECT	     4





      A.   SUMMARY OF OPERATIONAL ASSISTANCE	     4





      B.   PLANT PERFORMANCE EVALUATION	    13





 IV.   SUMMARY AND CONCLUSION	    14





  V.   RECOMMENDATIONS	    15





 VI.   REFERENCES	    17

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                               LIST OF FIGURES
        FIGURES                                                 PAGE NUMBER
1.   PLANT FLOW SCHEMATIC.

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 I.  INTRODUCTION







     On September 14, 1972,  Region VIII of the Environmental Protection Agency




 (EPA), received a letter from the Colorado Department of Health requesting




 operational assistance at the Upper Eagle Valley Sanitation District Waste-




 water Treatment Facility.  An on-site evaluation survey of the facility was




 conducted by EPA on October 26 and 27, 1972 and a formal technical assistance




 project was initiated on March 19, 1973.   This report outlines the findings




 and results of the technical assistance project and proposes several recommen-




 dations for future consideration at the Upper Eagle treatment plant.







II.  DESCRIPTION OF PLANT




    A.   BACKGROUND




    Vail, Avon, and the surrounding area is provided wastewater treatment by




 two separate sanitation districts.  The Vail Sanitation District (VSD)  serves




 primarily the Town of Vail and discharges its effluent into Gore Creek.  The




 Upper Eagle VAlley Sanitation District (UEVSD) serves localities upstream




 (the Big Horn Area) and downstream of the Town of Vail.  The UEVSD discharges




 its effluent to the Eagle River downstream of the confluence of the River with




 Gore Creek.




    Since a portion of the area served by the UEVSD is located upstream of the




 VAil facility, an agreement between the two districts was reached providing




 for a portion of Vail's collection lines to be used by the UEVSD to trans-




 port sewage to the Upper Eagle treatment plant.




    Flow from the Big Horn area is measured prior to entering the Vail inter-




 ceptors.  This flow is transmitted to the Vail plant along with sewage from

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Vail.  At the Vail facility the flow is split and an amount approximately




equal to that flow measured from the Big Horn area is directed to the UEVSD




plant.  Vail is required to pay the UEVSD for all wastewater sent to the UEVSD




plant in excess of that measured at the Big Horn metering station.   It is




noted that the interelationship that exists between the plants provides a




means to adjust flows to a desired quanity between the two facilities and




therefore must be considered an important operational tool.






    B.  PLANT FACILITIES







    Figure 1 shows a plant flow schematic of the Upper Eagle Wastewater




Treatment Facility.  Flow enters the facility and passes through a bar screen,




grit channel, parshall flume, and comminutor before entering the aeration




basin.  Flow continues through the aeration basin, final clarifier, and




chlorine basin before it is discharged to the Eagle River.  Sludge removed in




the final clarifier is collected by a vacuum type sludge scraper mechanism and




is returned to the aeration basin by a constant speed centrifugal pump.  Return




flow may be adjusted by opening or closing a plug valve located at the return




sludge discharge point in the aeration basin.  The pretreatment facilities




and/or the aeration basin and secondary clarifier may be bypassed by opening




and closing the appropriate gates and valves.




   Sludge is wasted from the bottom of the secondary clarifier through an




air lift pump to the aerobic digester.  Digested sludge is drained to a sludge




drying bed and digester supernatant is directed back to the aeration basin.




Dissolved oxygen and mixing is provided in both the aeration basin and




aerobic digester by air blowers coupled with surface and subsurface mechanical




agitators.

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     TECHNICAL ASSISTANCE PROJECT
UPPER EAGLE VALLEY SANITATION DISTRICT
     WASTEWATER TREATMENT FACILITY
            AVON, COLORADO
           MARCH-APRIL, 1973

         PLANT FLOW SCHEMATIC
  'Final Clarifier Effluents

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III.   SUMMARY OF ASSISTANCE PROJECT







       A.   SUMMARY OF OPERATIONAL ASSISTANCE







       At  Upper Eagle the primary emphasis  of  the  assistance  project was  on




  operational control of the facility.   No  formal  assistance  was  given on




  procedures used to conduct various  monitoring tests  such  as biochemical




  oxygen demand (BOD^)  and total suspended  solids  (TSS).  During  the project




  the BODg and TSS analysis were performed  by  an EPA chemist.  After comple-




  tion of  the Upper Eagle assistance  project a few BOD^ and TSS analysis




  were conducted by plant operators at.  the  Vail facility.




       Presently it is not feasible for plant  operators at  Upper  Eagle to




  routinely perform BOD^ and TSS analysis because  of the  limited  manpower




  available and lack of the necessary equipment at the facility.   The  necessary




  laboratory equipment should be purchased  to  enable plant  personnel to run




  selected monitoring analysis.




       Control over plant operation at  the  Upper Eagle Treatment  Facility




  involved conducting various "control" tests  and  interpreting the corres-




  ponding  results.  The control  tests used  were dissolved oxygen, centrifuge




  turbidity, settleability, and  sludge  blanket depth.  The  centrifuge  turbid-




  ity and  sludge blanket depth tests  were conducted four  times per day, seven




  days per week, the settleability test was conducted  two times"per day,  seven




  days per week, and the dissolved oxygen test was conducted  periodically




  during the assistance project.  After assistance the control tests were




  conducted twice per day during the  days when a plant operator was at the




  facility.




       The dissolved oxygen (D.O.)  tests ware  used to  monitor the D.O. concentration

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in the aeration basin and aerobic digester.   For both the aeration basin and




aerobic digester the D.O. test was used to insure that the D.O.  concentration




was maintained greater than 1 mg/1.




     The centrifuge tests were used to determine the variations  in solids




concentrations from day to day.  Tests were conducted on samples of mixed




liquor taken at the discharge end of the aeration basin, on samples of return




sludge, on samples of sludge in the aerobic digester, and on samples of sludge




wasted to the aerobic digester.  Although it is not necessary for control, a




correlation between percent solids by volume and solids by weight was made.




The results of this correlation indicate that during the project one




percent by volume was approximately equal to 1,000 mg/1 by weight.  This




correlation will vary as the characteristics of the sludge vary.  For this




report all solids concentrations by weight were determined using the correlation




of one percent by volume equal to 1,000 mg/1 by weight.




     The turbidity tests were performed on samples of clarified  supernatant




from the final clarifier.  Test results were used to monitor the performance




of the activated sludge process prior to obtaining a BOD^ result.




     The settleability tests were conducted on samples of mixed  liquor




collected at the discharge end of the aeration basin.  The tests were used




to monitor and observe sludge settling characteristics.




     Sludge blanket depth determinations were made on the final  clarifier.




Results were used to monitor the changes in the depth of the sludge blanket




and to determine the amount of sludge that was accumulating in the final




clarifier.




     Data obtained from the control tests were used to perform calculations




and develop gfaphs which were used to interpret plant performance and control

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plant operations.  After completion of the assistance project Upper Eagle




purchased all the necessary equipment to conduct the "control" tests and




are using the tests, calculations, and graphs to control plant operation.




     Initiation of process control pointed out various procedures that must




be used to control plant operations and in addition pointed out various




limitations in plant design which hindered plant performance.




     One of the major factors limiting performance was inadequate control




over the return sludge flow rate.  Return sludge flow control is necessary




to provide control of the MLSS concentration throughout the day as the sewage




flow rate varies.  This fact is increasingly important at Upper Eagle because




of the relatively short detention time in the aerator (4.5 hours at the design




flow of 4,163 cu m/day (1.1MGD))  for a plant of this type (i.e. no primary




clarifiers).




     Two major reasons for the lack of adequate return sludge flow control




are insufficient manpower provided at the facility and inadequate physical




control over the return flow rate.  Two plant operators are available to




cover plant operation eight hours per day, six days per week.  These same




operators; however, are responsible for the collection system and at times




cannot be at the treatment plant for even the limited time of eight hours




per day, six days per week.  To provide for adequate return sludge flow control




an operator must be at the plant to adjust the return flow rate during the




times when the sewage flow increases and decreases.  This normally represents




a minimum time of sixteen hours per day seven days per week for a plant of this




size.




     Sludge is returned to the aeration basin at Upper Eagle through one




constant speed centrifugal pump at a constant rate of approximately 3,785

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cu rn/day (1 MGD).




     This constant return rate represented a fluctuation in the return flow




percentage (i.e. ratio of return sludge flow rate to incoming sewage flow




rate) of about 85% to about 200%.  Before plant operators can control the




return flow rate there had to be a physical method developed to accomplish




the control.   During assistance two methods were developed to try and control




the return flow rate.  The first method involved using a pressure switch




activated by the liquid level in the return sludge wet well.  The second




method involved installing a plug valve on the return sludge discharge line




to the aeration basin.  This method of control was partially successful and




allowed the flow rate to be adjusted lower than the maximum output of the




return sludge pump.  Although the rate of flow of return sludge could be




adjusted the flow rate could not be measured.  No return sludge flow measuring




devices are provided at the Upper Eagle facility.  Attempts were made to




estimate the flow rate, but a good estimation could not be made.  It is




recommended that a flow measuring device be provided.




     Additional problems with return sludge flow adjustments were also




encountered after the plug valve had been installed.  The sludge collection




mechanism in the final clarifier at Upper Eagle is a vacuum type scraper




mechanism that has a center wet well connected to the sludge pick up ports.




The center wet well revolves around the fixed center support column.  The




joint between the support column and the wet well is sealed by a flexible




rubber gasket which is provided to prevent the mixed liquor that enters the




clarifier from leaking into the return sludge wet well.  During assistance




this seal was leaking and mixed liquor was allowed to dilute the return sludge.




The effects of this dilution became more and more pronounced as the return

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sludge flow was decreased.  For example, when the return rate was decreased




a greater percentage of the return flow consisted of mixed liquor and a lower




percentage consisted of settled sludge from the bottom of the clarifier.




Eventually the settled sludge in the clarifier became thicker and thicker




and plugged the sludge pick up ports.  At that point the return flow consisted




entirely of mixed liquor leading through the seal and no settled sludge in




the clarifier could be returned to the aeration basin.  Because of the limitation




caused by the leaky seal, the return sludge flow rate adjustments were very




ineffective in controlling the MLSS concentration in the aeration basin.




     It was pointed out by the plant operators that the leaky seal had been




repaired approximately one year prior to the assistance project.  It is




recommended that the seal be repaired once again and that in the future the




seal be checked at least twice per year and replaced when necessary.




     Another major plant deficiency that limits plant performance at Upper




Eagle is the size of the aeration basin.  The plant flow pattern is designed




in a similiar fashion to an extended aeration facility, (i.e. no primary




clarifier, one aeration basin).  However, at the average daily design flow




(4,163 cu m/day(l.l MGD)), the aeration basin detention time is 4.5 hours




rather than the 24 hours normally associated with extended aeration facilities.




The detention time at average flow during assistance  (2,649 cu m/day(0.7




MGD)) was 7.1 hours which is still significantly less than a typical 24 hours.




One of the disadvantages of designing a plant with conventional detention




times (i.e. 4-6 hours) and no primary clarifier is that settleable organic




material is recycled with activated sludge (i.e. it settles in the final




clarifier and is returned with the activated sludge to the aeration basin).






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This settleable organic material is in most cases more difficult to break




down by bacteriological activity and as a result must be recycled many times




in a system that has a short aeration time in order to achieve a stable end




product.  The effect is to overload the system and reduce the quantity of




settleable organic material converted to a stable end product and quantity




of colloidal and dissolved organic material converted to settleable sludge




solids.  An approach to increase these conversions is to carry a higher MLSS




concentration.  The higher MLSS concentration in part compensates for the




shorter aeration basin detention time.  The problem encountered in this




approach is that the size of the aeration basin (small) and final clarifier




(large) establishes an interrelationship that directly affects the systems




ability to maintain a selected "activated" MLSS concentration.  Generally a




small aerator is associated with systems that have lower MLSS concentrations




(high rate systems).




     Another limitation in plant design at Upper Eagle that indirectly affects




plant performance is the aerobic digester capability at the facility.  During




assistance the digester was not performing satisfactorily and as a result




removal of excess sludge from the activated sludge portion of the plant was




severely hindered.  The poor digester performance was characterized by a




sludge that would not develop a clear supernatant layer even after extended




periods of quiescense (i.e. 24 hours).  To allow room for waste sludge in




the digester, sludge had to be drawn to the snow covered drying beds.




Several factors which contributed to the inadequate digester performance




during the assistance project were excessive solids loading to the digester,




low temperature of the digester contents, and inadequate detention time in the




digester.

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     Approximately one week before and during the assistance project, large




quantities of sludge were wasted to the aerobic digester within a short time




period.  The purpose of wasting a large quantity of sludge within a short




time period was to aid in attaining the optimum MLSS concentration.  The




effect of the heavy solids loading to the digester was that normal digestion




appeared to be upset and adequate supernating in the digester was prevented.




Future plant operations should strive to achieve a balance in solids




distribution in the plant so that heavy solids loadings to the digester are




avoided.




     A second factor, low temperature in the digester, was felt to be the




leading cause of inadequate digester performance during assistance.  Frequently




the temperature of the sludge in the digester was so low that ice formations




were observed in and around the edges of the digester.  The low temperature




of the sludge caused the microorganisms to be less active and therefore




decreased the rate of sludge digestion.  A cover over the existing digester




would help this situation to a degree but other considerations such as an




external heat source or alternate means of ultimate sludge disposal must be




considered to compensate for the decreased sludge digestion rate caused by




lower temperatures.




     A thorough analysis of the detention time in the digester was not made




because sufficient data was not obtained during the project.  The design




detention time; however, is 5 days (2).  This design detention time is not




sufficient for adequate digestion.  It is recommended that a thorough analysis




be made of the detention time in the digester, with respect to adequate




digester performance, prior to initiating major modifications apparently




necessary at the Upper Eagle facility.  A suggested minimum detention time for
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an aerobic digester associated with a plant like Upper Eagle's is 20 days (3).




     Another limitation in plant design that degraded plant effluent quality




was the absence of a skimmer in the final clarifier.  No method of removing




floating material is available at the Upper Eagle facility and as a result




the plant effluent quality is degraded.  It is recommended that a skimming




device be provided.




     The plant limitations that have been outlined above inhibited the ability




to provide adequate operational control at the Upper Eagle facility.




Therefore, operational assistance turned into developing methods to make the




best of the required mode of operation.




     During the assistance project the sewage flow rate to the Upper Eagle




facility was increased because of the sever problems that were being




encountered with plant operation at the Vail Wastewater Treatment Facility.




Future operation of the Upper Eagle facility should include the capability




to reduce flow by letting Vail take on an additional volume of sewage.  This




interrelationship is a useful tool that must be fully developed between both




facilities.  It is noted that the increased flow at Upper Eagle during




assistance did cause a slight deterioration of plant effluent quality.




     The method of wasting activated sludge was modified to conserve digester




capacity and to account for the quanity of solids wasted.  As thick a sludge




as possible was wasted to the digester by shutting off the return sludge pump




and allowing the sludge to accumulate and concentrate in the secondary clarifier.




This sludge was then wasted to the digester at as slow a rate as possible.  It




is recommended that sludge continue to be wasted as thick as possible until




adequate digester performance is attained.  At that time a thick sludge should




continue to be wasted but the return sludge flow rate should not be stopped







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prior to wasting.   Each time sludge was wasted the concentration was




determined using the centrifuge.   The volume of sludge wasted was determined




by measuring the volume occupied by the wasted sludge in the digester.   Using




both the volume and concentration of sludge wasted the quantity of sludge




removed from the activated sludge system was determined.  It is recommended




that this method of determining the amount of sludge wasted be used in  future




plant operations.




      At the beginning of the federal assistance project, the Upper Eagle




plant was glutted with sludge solids which were being rapidly recycled




throughout the system by the constant high return sludge flow rate.  By




interpreting the control tests and by analyzing unit sizes various operational




changes were concluded.  In summary, it was decided to increase the MLSS to




as high a concentration as possible to obtain the best treatment using  the




minimum aeration basin detention time provided.  The approach to increasing




MLSS is outlined as follows:  Excess sludge was in the system and was hindering




the activated sludge's ability to dewater.  This excess sludge was wasted.  As




the excess sludge was wasted the settleability tests indicated that the




remaining sludge in the system dewatered much better to almost twice the




concentration as with prior tests in a given time period (i.e. 60 minutes).




A plug valve was installed so that return sludge rates could be decreased to




take full advantage of the sludge's ability to dewater and to limit the




quanity of excess water that was being recycled to the aeration basin.   This




mode of operation, if it had been successful, should have produced the  highest




effluent quality.   However, wasting limitations, inadequate return sludge




control, leaky seals in the clarifier, and other problems forced this method




of operation to be abandoned.
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     The return sludge flow rate, by necessity (i.e.  to prevent plugged




sludge pick up ports in the clarifier because of leaky seals),  was returned




to its original high rate and the maximum MLSS concentration was achieved




by allowing the solids in the system to build and still avoid bulking in




the final clarifier.  This method of operation is highly undesirable in




light of the control the operators could have if adequate facilities and




controls were available.




     B.  Plant Performance Evaluation







     During assistance plant performance at Upper Eagle was satisfactory,




(effluent BOD^ and TSS was approximately 25 mg/1 except during the higher




flow period as explained above when effluent BODg and TSS was about 40 mg/1).




However, it is felt that a consistent, high'-quality effluent would be difficult




to maintain due to inadequate control over the treatment plant operation and




limitations in plant design.  Inadequate control over plant operation was




due primarily to inadequate control over the return sludge flow rate.  Control




over the return flow rate was not provided because of limited manpower




available at the plant, leaky seals in the final clarifier, and inadequate




physical control .over the return rate itself.  Physical control over the




return rate was provided during the assistance project by placing a plug




valve on the return sludge line.  Using the plug valve the return sludge flow




rate can be adjusted.  The adjustments; however, cannot be used to adequately




control plant operation until the leaky seals in the clarifier are repaired




and adequate manpower at the plant is provided.  It should also be noted that




only one return sludge pump is provided at Upper Eagle.  It is apparent that




if repairs are required on that pump the entire return sludge flow capability




is eliminated and plant effluent quality would deteriorate.  To prevent complete
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elimination of the return sludge capability during periods of pump maintenance




it is recommended that a separate return sludge pump be provided at Upper




Eagle.  It is also recommended that the leaky seals in the clarifier be




repaired and that adequate plant staffing be provided.  At that time the plug




valve or some other method of controlling the return flow rate should be used




and plant operation should be controlled in order that the most consistent,




highest quality effluent be attained with the facilities available.




IV.  SUMMARY AND CONCLUSIONS




     Region VIII of the Environmental Protection Agency received a letter




from the Colorado State Department of Health requesting assistance concerning




the operation of the Upper Eagle Valley Wastewater Treatment Facility.  An




initial evaluation of this plant was made on October 26, 1972 and a formal




technical assistance project was initiated on March 19, 1973.




     During assistance, plant personnel were given instruction in conducting




and interpreting various process control tests.  Results from these tests




pointed out various procedures that must be used to control plant operation




and in addition pointed out various limitations in plant design which hindered




plant performance.




     One of the major factors limiting plant performance was inadequate control




over the return sludge flow rate.  A plug valve was installed so that the




return rate could be physically adjusted; however, limited manpower at the




facility and a leaky seal in the clarifier prevented attempts to control this




rate.  In addition to this lack of return control, the return flow rate could




not be measured.




     Another plant deficiency that limits plant performance is the size of




the aeration basin.  The basin is too small for the type of facility that




exists at Upper Eagle and a consistently high quality effluent would be






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difficult to achieve and maintain.   In future plant modifications consideration


should be given to expanding the aeration basin facilities.


     Inadequate digester performance indirectly affected plant performance


during the assistance project.   The reasons for poor performance were cold


temperature of the digester contents, inadequate detention time in the digester,


and excessive solids loading to the digester.  Present digester performance


can be improved by providing proper wasting control of excess activated


sludge and by modifying the digester to include placing a cover over the


digester and possibly providing an external heat source to heat the digester


contents.  An alternate means of ultimate disposal should also be considered.


In addition expansion of the digester capacity to allow for a longer sludge


detention time appears to be necessary.


     Another plant limitation at Upper Eagle is that no method of removing


floating material is available.  The obvious effect of this, limitation is


a degraded plant effluent.


      Although various operational changes were initiated during the Upper


Eagle assistance project, plant deficiencies inhibited proper operational


control.  This lack of operational control limited the improvement of


effluent quality and required an operational mode to be continued that was

   /
highly undesirable.



V..  RECOMMENDATIONS



     Based on the results of the technical assistance project the following


recommendations are made:


     1.  Purchase the necessary laboratory equipment to enable plant personnel


to run selected monitoring analysis.



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     2.  Provide a flow measuring device on the return sludge flow line so




that the flow rate can be accurately measured.




     3.  Repair the leaky seal in the final clarifier as soon as possible




and in the future check the seal at least twice per year and replace it




when necessary.




     4.  Maintain the relationship between the Vail and Upper Eagle Treatment




Facilities so that additional flow can be accepted at one facility when the




other is experiencing operational difficulties.




     5.  Provide an alternate return sludge pump that can be used when the




existing pump is out of service.




     6.  Future plant expansion at Upper Eagle should include consideration




of enlarging the existing aeration basin capacity.  In the interim period




a lower flow capacity would be desirable.




     7.  To aid present digester performance a cover should be placed over




the digester.  Also consideration should be given to providing an external




heat source or an alternate means of ultimate sludge disposal to insure




continued operation in winter months.  Any plant expansion should investigate




the sludge detention time in the existing digester which is believed to be




inadequate.




     8.  Place a shimmer on the final clarifier to remove floating material




from the waste stream.




     9.  Provide adequate plant staffing to control plant operation during




periods of increasing or decreasing sewage flow or for a minumum of 16 hours




per day, 7 days per week.




    10.  Continue conducting the operational control tests and operational




practices that were initiated during the assistance project.
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VI.  REFERENCES







      1.  "Operation and Maintenance Manual,  Sewage Treatment Plant,  Upper




 Eagle Valley Sanitation District".




      2.  "Process Design Manual for Upgrading Existing Wastewater Treatment




 Plants" prepared for the U. S.  Environmental Protection Agency by Roy F.




 Weston, Incorporated, Contract No.  14-12-933, U.  S. Environmental Protection




 Agency, Region VIII, Denver, Colorado  80203 (October, 1973).
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