EPA-600/2-77-165
August 1977
Environmental Protection Technology Series
              MAGNESIA FGD PROCESS TESTING
                ON A COAL-FIRED POWER PLANT
                               Industrial Environmental Research Laboratory
                                    Office of Research and Development
                                   U.S. Environmental Protection Agency
                               Research Triangle Park, North Carolina 27711

-------
                    RESEARCH REPORTING SERIES
Research reports of the Off ice of Research and Development, U.S. Environmental Protec-
tion Agency have been grouped into nine series. These nine broad categories were
established to  facilitate further development  and application of environmental tech-
nology. Elim nation of traditional grouping was consciously planned to foster technology
transfer and a maximum interface in related fields. The nine series are:

          1 Environmental Health Effects Research
          2 Environmental Protection Technology
          3 Ecological Research
          4 Environmental Monitoring
          5 Socioeconomic Environmental Studies
          6 Scientific and Technical Assessment Reports (STAR)
          7 Interagency Energy-Environment Research and Development
          8 "Special" Reports
          9 Miscellaneous Reports

This report has been assigned to the ENVIRONMENTAL PROTECTION TECHNOLOGY
series. This series describes research performed to develop and demonstrate instrumen-
tation, equipment, and methodology to repair or prevent environmental degradation from
point and non-point sources of pollution. This work provides the new or improved tech-
nology required for the control and treatment of pollution sources to meet environmental
quality standards.
                             REVIEW NOTICE
This report has been reviewed by the participating Federal Agencies, and approved for
publication. Approval does not signify that the contents necessarily reflect the views and
policies of the Government, nor does mention of trade names or commercial products
constitute endorsement or recommendation for use.

This document is available to the public through the National Technical Information
Service, Springfield, Virginia 22161.

-------
                                             EPA-600/2-77-165
                                                  August 1977
MAGNESIA  FGD  PROCESS TESTING
 ON  A COAL-FIRED  POWER  PLANT
                          by

                     Diane K. Sommerer

                   York Research Corporation
                    • One Research Drive
                   Stamford, Connecticut 06906
                    Contract No. 68-02-1401
                   Tasks No. 1, 10, 24, and 25
                   Program Element No. 1AB013
                      ROAP No. 21BAV
               EPA Project Officer: Charles J. Chatlynne

              Industrial Environmental Research Laboratory
                Office of Energy, Minerals, and Industry
                 Research Triangle Park, N.C. 27711
                       Prepared for

               U.S. ENVIRONMENTAL PROTECTION AGENCY
                 Office of Research and Development
                    Washington, D.C. 20460

-------
ABSTRACT
This field measurement program was initiated with the overall ob-
jective of determining the operability and reliability of the
Chemico magnesium oxide venturi scrubber in operation at Potomac
Electric Power Company's Dickerson Generating Station, located in
Frederick , Maryland.

To achieve this objective, a continuous source-monitoring station
was installed at the scrubber, and was complemented by a field
analytical laboratory intended for the measurement and analysis
of various process streams.  These facilities continuously monitor-
ed process and emission variables during a four month period between
October 1974 and January 1975; and later during the month of August
1975.

Scrubber operation was evaluated during periods of steady-state opera-
tion, and transient operation.  The latter included periods of start-
up, shutdown, and malfunction.  During the test period, the scrubber
was available for approximately 48 percent of the time.  This per-
cent availability included all levels of operation, steady-state
and transient alike.  It is estimated that of the time that the sys-
tem was available, approximately 80 percent was steady-state where
the system was operating normally.

This test program showed that, although scrubber availability was
not all that was desired due to problems with logistics in supplying
raw materials (MgO), and to mechanical problems mainly attribu-
table to under-design in such areas as piping, slurry pumps, and
other auxiliary equipment, the basic scrubber concept and design was
one that should meet critical criteria once these problems are
remedied.
                                111

-------
                        ACKNOWLEDGEMENTS
York Research Corporation wishes to express its appreciation to
the Potomac Electric Power Company's Dickerson Generating Station
personnel for their cooperation during the test program.  Appre-
ciation is extended also to Dr. Charles Chatlynne and Mr. Robert
Hendriks of the Industrial Environmental Research Laboratory -
Research Triangle Park (IERL-RTP), and to,the Chemical Construc-
tion Company (Chemico).
                               -iv-

-------
                            CONTENTS


                                                       Page

     ABSTRACT                                           iii

     ACKNOWLEDGEMENTS                                    iv

     FIGURES                                            Vii

     TABLES                                            viii

     SUMMARY                                             ix

1.0  INTRODUCTION                                         1

2.0  PLANT DESCRIPTION                                    3

3.0  FGD SYSTEM PROCESS DESCRIPTION                       5
     3.1  First Stage - Flyash Removal                    9
     3.2  Second Stage - SO2 Removal                      9
     3.3  Solids Concentration                           10
     3.4  Drying                                         10
     3.5  Dry Solids Storage                             10
     3.6  Calcination                                    10
     3.7  Scrubber Process Control                       11

4.0  TEST PROGRAM                                        13
     4.1  Test Methods                                   13
          4.1.1  Continuous Monitoring Program           13
          4.1.2  Measurement of Process Streams          15
          4.1.3  Manual Testing of Gaseous Emissions     19
          4.1.4  Instrument Calibration                  19
          4.1.5  Operational Data                        20
     4.2  FGD System Availability                        21
     4.3  Boiler and ESP Availability                    22

5.0  TEST RESULTS                                        25
     5.1  Boiler and ESP                                 25
     5.2  Scrubber:  Steady-State Operation              25
          5.2.1  Scrubber First Stage                    25
          5.2.2  First Stage Bleed                       29
          5.2.3  Thickener Overflow                      31
          5.2.4  Thickener Underflow                     31
          5.2.5  Scrubber Second Stage                   32
          5.2.6  MgO Slurry                              35
          5.2.7  Second Stage Bleed                      36
          5.2.8  Centrifuge Cake                         38
          5.2.9  Mother Liquor                           38
          5.2.10 Dryer Product                           39
     5.3  Scrubber:  Transient Operation                 40
          5.3.1  Startups                                40
          5.3.2  Shut-Downs                              42
          5.3.3  Malfunctions                            42
          5.3.4  Leaks                                   46
          5.3.5  Centrifuge Outages                      46

                                 -v-

-------
5.3.6  First Stage Outages
5.3.7  Second Stage Outages
                                              50
                                              50
6.1.2
6,
6,
6.1.5
,1.3
,1.4
6.0  ENGINEERING EVALUATION                              53
     6.1  Operability                                    53
          6.1.1  Scrubber First Stage                    53
                 Solids Removal Section for the First
                 Stage                                   57
                 Scrubber System Second Stage            57
                 MgO Slaking and Recycle                 59
                 Solids Removal Section for the          60
                 Second Stage
          6.1.6  Process Control                         66
     6.2  Optimization                                   67
          6.2.1  Second Stage Absorber                   67
          6.2.2  MgO Slaking                             80
          6.2.3  Solids Removal System                   82
     6.i)  Performance                                    84
          6.3.1  SO2 Removal Efficicney                  84
          6.3.2  Particle Removal Efficiency             85
          6.3.3  Duration of Scrubber Performance        86

7.0  CONCLUSIONS                                         87

     REFERENCES                                          89

     APPENDICES

  A. SCHUBBER EQUIPMENT LIST AND EQUIPMENT
     SPECIFICATIONS

  B. TABULATION OF DATA

  C. DAILY OPERATING LOGS

  D. METHODOLOGY

  E. TR*NSIENT CONDISTIONS

  F. LIST OF SCRUBBER MALFUNCTIONS AND MAINTENANCE
                       -VI-

-------
                             FIGURES

                                                      Page


3-1. SCHEMATIC DIAGRAM OF CHEMICO WET                   6
     SCRUBBER SYSTEM

3-2. BOILER-SCRUBBER CONFIGURATION                      7

3-3. FLOW DIAGRAM OF THE FGD SYSTEM                     8

4-1. SAMPLING LOCATIONS                                14

5-1. DRYER PRODUCT Fe203: 11/10/74                     41

6-1. S02 REMOVAL EFFICIENCY DURING CENTRIFUGE OUTAGE
     (11/15/74)                                        62

6-2. LIQUID FLOW RATE VARIATION; 12/17/74              71

6-3. HIGH GAS FLOW; 1/27/75                            73

6-4. UNREACTED MgO IN CENTRIFUGE CAKE AS A FUNCTION
     OF TEMPERATURE
                                                       81
                                -vii-

-------
                             TABLES




                                                        Page




4-1. SCRUBBER CHARACTERIZATION TESTING PROGRAM         16r-18




4-2. VALIDATION OF INSTRUMENTAL DATA                      20




5-1. BOILER OPERATING PARAMETERS                          26




5-2. SCRUBBER FIRST STAGE OPERATING PARAMETERS         27-28




5-3. SCRUBBER SECOND STAGE OPERATING PARAMETERS        33-35




5-4. PERCENT S02 REMOVAL AT SHUT-DOWN                     43




5-5. SUMMARY OF MAJOR TRANSIENT CONDITIONS             44-45




5-6. LEAKS NOV., DEC. '74; JAN., AUG. '75                 47




5-7. CENTRIFUGE REPAIR                                    48




5-8. CENTRIFUGE PERFORMANCE                               49




5-9. FIRST STAGE OUTAGE                                   50




5-10.SECOND STAGE OUTAGE                                  51




6-1. LEAKS OF THE SCRUBBER SYSTEM      *                   55




6-2. FIRST STAGE OUTAGE; DEC. 7, 1974                     56




6-3. SECOND STAGE OUTAGE; DEC. 16, 1974                   59




6-4. BOILER/SCRUBBER DATA; NOV. 15, 1974                  63




6-5. PERCENT SOLIDS                                       64




6-6. CENTRIFUGE REPAIR                                    65




6-7. BOILER/SCRUBBER DATA                                 68




6-8. BOILER/SCRUBBER DATA                                 69




6-9. LIQUID FLOW RATE CHANGES; DEC. 17, 1974              72




6-10.BOILER/SCRUBBER DATA                              74-75




6-11.TEST RESULTS; DEC. 17, 1974                          77




6-12.BOILER/SCRUBBER DATA                              78-79




6-13.ALTERATION OF Ap                                    80




6-14.SOLIDS REMOVAL EFFICIENCY DATA                       83




     CONVERSION FACTORS:  BRITISH TO SI UNITS             90




                                -viii-

-------
SUMMARY

This report presents the results of a five-month study of an 95 MW
MgO Demonstration FDG System on a coal-fired utility boiler.  The
site chosen for this study was the Dickerson Generating Station
which is operated by Potomac Electric Power Company.  This facility
had been fitted with a Chemico/Basic Two-Stage MgO Venturi scrubber.

This test program showed that, although scrubber availability was
not all that was desired due to problems with logistics in supply-
ing raw materials (MgO), and to mechanical problems mainly attribu-
table to under-design in such areas as piping, slurry pumps, and
other auxiliary equipment, the basic scrubber concept and design was
one that should meet critical criteria once these problems are
remedied.

This report discusses scrubber operation during steady-state and
transient operating conditions, and the basic chemical character-
istics of the process streams.  Recommendations are provided re-
lative to the unit's operation and maintenance from the viewpoint
of improvements in mechanical design to improve the availability.

Due to the limited availability during the test program which did
not provide the opportunity for full system characterization and
optimization, and to the system's indicated strengths, recommenda-
tion is given that further testing of the MgO FGD System be carried
out in order to better characterize the process.
                               -ix-

-------
-x-

-------
1.0  INTRODUCTION

York Research Corporation (YRC) was contracted by the Industrial
Environmental Research Laboratory - Research Triangle Park (IERL-RTP)
of the Environmental Protection Agency (EPA) to perform a test pro-
gram upon a Magnesia Flue Gas Desulfurization (FGD) process on a coal-
fired utility boiler.  The objectives of the program were to charac-
terize both emissions from,  and the process operation of, the FGD
system under both steady-state and transient operating conditions.
This was to be achieved through the installation and operation of
a continuous emission monitoring program, which was supplemented by
manual emission measurements using standard EPA techniques, and
by the sampling of certain process streams.

The site chosen for the test program was the Dickerson Generating
Station, operated by the Potomac Electric Power Company  (PEPCO).
This station had been equipped with a Chemico/Basic MgO FGD demon-
stration scrubber system.

Mr. Roland Glenn of Combustion Processes, Inc. was involved in the
program as a field consultant for the purpose of assisting with
process evaluation.

During the test program, PEPCO plant operators and the Chemical
Construction Company were responsible for the operation, optimiza-
tion, repair, and maintenance of the demonstration system.  Data
presented in this report are results of YRC's observations and
measurements made during the program.

The test program commenced in October 1974 and ran continuously
until the end of January 1975.  At that time, there was a scheduled

                               -1-

-------
outage for boiler repairs.  Dior ing this period, a considerable amount
of repair work was performed upon the FGD system.  In August 1975,
the test program was resumed and ran until the end of the month,
at which time it was terminated due to lack of further committment
on the part of PEPCO to supply the additional necessary maintenance
funds.  The U.S. EPA did have funds allocated for the continuation
of the operation of the regeneration facility.

The objectives of the program were to characterize scrubber emissions
and variations in emissions, as well as the performance factors
of the FGD process during:
     •  Steady-state operating conditions
     •  Transient operating conditions
Steady-state conditions are defined as being in effect when the flue
gas flow, boiler operating conditions, and fuel constituents were
not fluctuating, and when scrubber process streams were in an equili-
brium state.

Steady-s*:ate conditions were determined to be in effect when after
startup, the scrubber had settled down into its normal operating
process condition.  Conversely, transient conditions were when this
mode of operation was not in effect (e.g., during scrubber startup,
shutdown, or malfunction).
                               -2-

-------
2.0  PLANT DESCRIPTION

The No. 3 boiler at PEPCO's Dickerson Generating Station is a
tangentially fired, pulverized coal-fired unit rated at 190 MW
(maximum continuous rating).  It was installed by Combustion
Engineering in 1962 and is designed to produce 1,300,000 pounds
of steam per hour at 2480 Ibs /in  at 1000°F superheat.  The unit
incorporates a separated twin furnace design with economizers,
waterwalls and generating surfaces, two stage superheat with spray
attemperation, reheat, and provision for dry bottom ash removal.
Four Raymond Bowl Mill Pulverizers feed 32 tangential burners;
i.e., one burner at each of the four levels at each furnace corner.
The boiler is equipped with two steam coil air heaters, and two
Ljungstrom rotary air heaters for combustion air preheat.  There
are two forced draft  (FD) and induced draft (ID) fans for con-
trolling furnace pressure and airflow, two forced circulation
pumps to maintain water flow, and a Bailey combustion control
system.  The boiler is also provided with pilot and warmup oil
torches (No. 2 Oil) which can be used as load carrying burners dur-
ing periods of firing low volatile or wet coal.

A Research Cottrell electrostatic precipitator  (ESP) is installed
in the exhaust gas network of boiler Unit No. 3 downstream of the
combustion air preheater.  This unit consists of two Opzel plate
precipitators in the same housing,, separated by an internal partition,
Each precipitator is divided into 2 units containing 3 sections of
6 foot plates along 21 ducted segments, with discharge electrodes
(wires) suspended between parallel plate collectors.  Twelve Syntron
vibrators are used on the discharge electrodes and 24 magnetic im-
pulse rappers (continuous cycle) are used on the collection plates
to dislodge collected matter.  Each unit is designed for a particle
removal efficiency of 97.5 percent, at design flow rate of 492,000

-------
cubic feet per minute (CFM) at 245 p.  Boiler exhaust qases typi-
cally contained the following:
     •  13.0 percent C02
     •   0.2 percent CO
     •   6.0 percent Q^
     •  6-10 percent moisture
A typical analysis of the bituminous coal which is fired at the
Dickerson Station shows the following:
        Heat Content
        Nitrogen
        Carbon
        Hydrogen
        Chlorine
        Sulfur
        Oxygen
        Moisture
        Ash
12,154 Btu/lb.
 0.96%
71.30%
 4.20%
 0.10%
 1.60%
 4.90%
 1.40%
15.42%
                                -4-

-------
3.0  FGD SYSTEM PROCESS DESCRIPTION

The Chemico/Basic Magnesium Oxide Flue Gas Desulfurization (FGD)
system (Figure 3-1)  was designed to accomodate approximately one-
half (295,000 ACFM at 259°F) of the exhaust gas from Unit No. 3.
This FGD system incorporated the following major processing steps:
                   •  Flyash removal
                   •  SO2 removal
                   •  Solids concentration
                   •  Drying
                   •  Dry solids storage
                   •  Calcination
The first five of the above steps were accomplished within the
system, while the last was carried out at the Essex Chemical
Company's sulfuric acid plant in Rumford, Rhode Island.

The total boiler-scrubber system configuration is shown in Figure 3-2,
where it is noted that appropriate by-passes were provided such
that gas flows to both the scrubber and ESP could be adjusted to
control the flow through each unit.

In its operating mode, the flue gas from the boiler was drawn into
the scrubber by means of an induced draft (ID) fan which was regulated
by the scrubber operators.  This permitted adjustment of the volume
of flue gas entering the scrubber inlet.  Design flow of the scrub-
ber was approximately 295,000 ACFM, which was about one-half of the
full load gas flow of the boiler.  The flow diagram for the entire
scrubber is shown in Figure 3-3.

The FGD system was designed as a two stage system, with the first
stage providing flyash removal and the second stage SO2 removal.

                                -5-

-------
             FLUE GAS IN
SCRUBBING
WATER iW
                         PLUMB  SOS
                                  DRYER EXHAUST GAS	
                                    CENTR/FU6ESOL/OS OUT
                                         MOTHER
                                         LIQUOR
                                          OUT
             Mg SO,
           TO  STORAGE
TO STACK      SILO
1 	 1
DILUTION
TANK
CLEAR WATER



\ \

L~~

1
	
SETTLING
POND
          SCHEMATIC DIAGRAM OF CHEMICO  WET SCRUBBING SYSTEM
                        UNIT NO. 3, PEPCO-DICKERSON
                                Figure 3-1
                               -6-

-------
                                                                       STACK
BOILER
PRECIPITATOR
;                                                                             SCRUBBER
                                                                             FAN
                        BOILER-SCRUBBER CONFIGURATION

                                   FIGURE 3-2

-------
                                  nastAu

                                    scuun
i
oa
I
                                                                                                     tarniw
HIW noa
                                        FLOW  DIAGRAM OF  THE FGD  SYSTEM



                                                   FIGURE 3-3

-------
3.1  First Stage - Flyash Removal
     The first stage was an adjustable throat venturi, where
     the flue gas was cooled from 250°F to 120°F and saturated
     with water vapor.  This stage was used for flyash (particle)
     control only, and its re-circulating liquid stream was
     separate and independent from that of the second stage.
     Ash-laden water was circulated at a nominal 2 percent
     solids concentration.  The adjustable venturi automatically
     controlled the first stage pressure drop/ which was main-
     tained at 11 inches (H2O).  Design particle removal ef-
     ficiency was 99.0 percent.

     A 980 gal /min   (GPM) bleed stream from the first stage
     recycle line carried ash to the thickeners.  A flocculant
     was used to aid settling in the thickeners.  Thickener
     underflow (20 GPM at 40 percent solids) was discharged to
     a dilution tank where water was added, and the mixture
     pumped back to a settling pond.  The overflow cascaded
     through a total of four ponds in series, and the water
     from the lowest pond was then pumped back to the dilution
     tank.  The thickener overflow was pumped back into the
     scrubber's first stage.  This closed-loop operation was
     maintained within first stage operation.

3.2  Second Stage - SO, Removal
     Flue gas, after leaving the first stage, passed upward
     through an annular mist eliminator, and then downward
     through the scrubber's second stage.  Within the second
     stage, magnesium oxide (MgO) was added to the scrubbing
     water.  This allowed the S02 in the flue gas to diffuse
     into the water droplets,  thus removing it from the gas
     stream.  In this process,  the S02 chemically reacts with
     the MgO, forming hydrated magnesium sulfites (MgSC^^nH-O) ,
     and to a lesser degree, magnesium sulfate (MgS04).

     Flue gas and entrained liquor entered the separator
                          — 9 —

-------
     portion of the absorber through a central downcomer.
     The liquor fell to the lower section of the separator
     which served as an integral storage reservoir,  while
     the gas passed upward through the second stage  mist
     eliminators and was exhausted through the stack to the
     atmosphere.

3.3  Solids Concentration
     A 170 GPM bleed from the absorption system entered a
     36 inch by 72 inch solid bowl centrifuge where  hydrated
     magnesium sulfite and magnesium sulfate crystals, and un-
     reacted MgO were separated from the mother liquor.  The
     mother liquor was returned to the second stage  absorption
     system, and the centrifuged wet cake entered the dryer.

3 o 4  Drying
     The wet cake containing hydrated magnesium sulfite,
     magnesium sulfate, MgO and surface moisture was dried
     by direct firing to remove free and combined moisture.
     Exhaust gas from the dryer passed through a cyclone dust
     collector, and back into the scrubber's second  stage.

3.5  Dry Solids Storage
     The anhydrous MgSO^ and MgSO^ material was conveyed from
     the dryer to a storage silo (capacity:  200 tons) where
     it was kept until it was transported to the sulfuric-acid
     plant for calcination.

3.6  Calcination
     The dry cake was transported to the Essex Chemical
     Company's sulfuric acid plant in Rumford, Rhode Island
     for calcination.  Regenerated MgO was returned (with
     make-up) and stored in the MgO silo (capacity:   100 tons),
     The MqO slurry was prepared using regenerated MgO, make-
     up MgO, and mother liquor.  This MgO slurry was added as
     make-up to the absorption recycle liquid circuit  (second
     stage).

                          -10-

-------
3.7  Scrubber Process Control
     The control process for this FGD system was relatively
     simple.  Basically/ the liquid flow rates through the
     scrubber were constant and independent of gas load.  The
     first stage of the venturi was automatically adjusted to
     maintain an 11 inch (I^O)  pressure drop across the venturi.
     MgO additive feed rate was varied to maintain the slurry
     pH at a preset point;  generally about 7.  The pH was
     measured at the discharge of the second stage re-circulation
     pump.  A downward pH trend triggered the addition of MgO
     to the system from the MgO make-up tank.
                          —11 —

-------
-12-

-------
4.0  TEST PROGRAM

During the five months that YRC test personnel were on-site, the
followina types of testing were performed:
         •  Continuous monitoring of scrubber emissions
         •  Measurement of process streams
         •  Manual testing of gaseous emissions.
Figure 4-1 illustrates the sampling points.

In the planning stage of the project, it was decided to continuous-
ly monitor CO, C02, and 0? as indicators of the status of boiler
operation, and to provide information regarding leaks in the FGD
system.  Once the program was underway, it became evident that CO/
concentrations were maintained at a level so low that instrumental
analytical values were unreliable.  Thus, after the first few weeks,
monitoring of this parameter was discontinued.  Oxygen, on the
other hand, proved to be a reliable indicator since its level was
well maintained within tight bounds in the combustion zone.

     4.1  Test Method
     4.1.1  Continuous Monitoring Program
          Gaseous effluent from the scrubber was continuously
          monitored during the program to obtain data related
          to the scrubber's performance during steady-state and
          transient operating conditions.  A continuous monitor-
          ing trailer was installed at the base of the scrubber
          approximately 45 feet from the ducting where the probes
          were situated.  Flue gas, after passing through a series
          of filters, was carried to the continuous monitoring in-
          struments by means of a heated sample line.  The gas
          flow was conditioned (where moisture was removed) in the

                               -13-

-------
  COAL
                BOILER
                               PRECIPITATOR/SCRUBBER  -  ABSORBER
                                  ADDITIVE SYSTEM FOR  SO^ RECOVERY
                                    SCHEMATIC PROCESS FLOW SHEET
                                 **^~
                                                                            • FUEL BURNERS
                                                                            • STEAM COIIS
                          TO DRY ASM HANDLING SYSTEM    HOT FAN
 RECYCLED
POND WATER
                            MgO FROM ACID PLANT
MgSOj TO ACID PLANT
                                           SAMPLING LOCATIONS

                                             FIGURE 4-1

-------
     trailer before passing to the instruments.   Flue gas
     samples were drawn alternately and sequentially from the
     inlet and outlet of the scrubber for periods of between
     5-20 minutes each.  Switching from one location to another
     was done automatically by a timer-solenoid switching sys-
     tem.  The sampling duration from either inlet or outlet
     were manually adjustable by the trailer operator.  This
     feature allowed shorter sampling times per point during
     transient conditions than during steady-state conditions.

     The parameters measured and the measurement principles
     were as follows:
      Parameter          Method          Instrument
      S02         Pulsed Fluorescence  Thermo Electron
                                       Model 40
      NO          Chemiluminescence    Thermo Electron
                                       Model 10B
      CO2, CO     NDIR                 Infra-Red Model 703
      09          Paramagnetic         Cleveland-Kent
                                       Model CKA-1A
      Flow             -  -            Teledyne-Hastings
      Temperature; Thermocouple              - -

     Detailed information concerning instrument operation
     appears in Appendix D.

4.1.2 Measurements of Process Streams
     The sampling and analytical program included the col-
     lection of data relative to the performance and relia-
     bility of the process itself.  All of the major process
     streams were studied and, in addition, some special
     investigations were made to study various secondary reac-
     tions and products.  Table 4-1 illustrates the scope of
     this part of the program.  Detailed information concern-
     ing the analytical methods used appears in Appendix D.
                          -15-

-------
                          TABLE 4-1.
               SCRUBBER CHARACTERIZATION TESTING PROGRAM
    Sampling Location
        Parameter
Location**   Sampling Frequency
    Analytical
Method  (Appendix
Bleed
Thickener Overflow
Thickener Underflow
SECOND STAGE

Bleed
Mother Liquor
pH
Magnesium
Suspended Solids
Chloride
Sulfate
Sulfite

Suspended Solids
pH
Chloride

Suspended Solids
pH
Chloride
pH
% Solids
% Mg S03-6 H20
% Mg S04
% MgO (Solids)
% MgO (Total)
Density

% Solids
% Mg S03.6 H20
% MgO (Solids)
% MgO (Slurry)
Density
                   8 hours
                      it

                      Tl

                      II


                      tl

                      II

                      IT


                      It

                      tf

                      II
                   4 hours
                      it

                      it

                      Tt

                      tt


                      tt

                      tt

                      tt

                      tt

                      tl
  Electrode
  Volumetrically
  Gravimetrically
  Turbidimetrically
  Colorimetrically
  Volumetrically
  Gravimetrically
  Electrode
  Turbidimetrically

  Gravimetrically
  Electrode
  Turbid imetrically
  Electrode
  Gravimetrically
  Volumetrically
  Colorimetrically
  Volumetrically
  Volumetrically
  Gravimetrically
  Gravimetrically
  Volumetrically
  Volumetrically
  Volumetri cally
  Gravimetrically
    Sampled only during the last month of scrubber evaluation (Aug.  1975).
    Determined during first portion of the program only (Oct., 1974 through Jan., 1975)
    Sampling Location - See Figure  4-1

-------
                    TABLE  4-1.  SCRUBBER CHARACTERIZATION TESTING PROGRAM  fCONT'O.)
   Sampling Location
      Parameter
Location**   Sampling Frequency
                   Analytical
               Method (Appendix D)
MgO Belt
Centrifuge Cake
Dryer Product
SPECIAL ANALYSES

Dryer Product
Second Stage Slurry

Scrubber 1st Stage
% MgO
% Mg

Density
% Combined Water
% Free Water
% Mg S03
% Mg SO 4.
    6


    7
4 hours
   Tt
                         % MgO
% Water
% Mg S03
% Mg S04
% MgO
Density
Iron Content

Trihydrate-
Hexahydrate Study

Time Dependance of pH
Sulfate
Sulfite
Chloride
Iron
Magnesium
pH
   tl

   tl

   It

   Tt

   ft

   tl


   tt

   tt

   tl

   tt

   tt
             November 10,11,1974
             2 Hour intervals

             Dec. 1974, Jan. 1975

             Dec., 1974

             Jan. 10, 1975
                   tt
Gravimetrically
Colorimetrically

Gravimetrically
Moisture Balance
Gravimetrically
Volumetrically
Colorimetrically
Volumetrically

Moisture Balance
Volumetrically
Colorimetrically
Volumetrically
Gravimetrically
                Colorimetrically


                Volumetrically

                Electrode
                Colorimetrically
                Volumetrically
                Turbidimetrically
                Colorimetrically
                Volumetrically
                Electrode
**
    Sampling Location - See Figure 4-1.

-------
                          TABLE  4-1.
SCRUBBER CHARACTERIZATION TESTING PROGRAM rCONT'O.)
oo
I
Sampling Location
Centrifuge Cake
Dryer Product
FIRST STAGE
Process Water
SECOND STAGE

Scrubber Inlet

Scrubber Outlet

Parameter
Water Content
Inert Material
Magnesium
Chloride
Iron
Chloride
SO 2
co2
°2
Flow
Temperature
SO2
CO 2
°?
Flow
Temperature
Location**
7
7
1
1
4
4
9
9
9
9
9
10
10
10
10
10
Sampling Frequency
August, 1975
August, 1975
August, 1975
August, 1975
August, 1975
August, 1975
Continuous
Continuous
Continuous
Continuous
Continuous
Continuous
Continuous
Continuous
Continuous
Continuous
Analytical
Method f Appendix D)
Moisture Balance
By Difference
Volume tri cally
Turbid imetrically
Colorimetrically
Turbidimetrically
Pulsed Fluorescent
NDIR
Paramagnetic
Pulsed Fluorescent
NDIR
Paramagnetic
       ** Sampling location - See Figure  3-1.

-------
4.1.3  Manual Testing of Gaseous Emissions
     Testing of the scrubber at its inlet and outlet was
     performed periodically during the test program using
     EPA Standard Methods.   This was carried out to validate
     the results obtained from the continuous monitoring in-
     struments.  Table 4-2  summarizes the comparative data
     obtained in this manner.  More detailed information
     appears in Appendix D.

4.1.4  Instrument Calibration
     All analyzers were calibrated daily in the manner spec-
     ified by the manufacturer of the instrument.  Calibration
     gas was stored in the  rear of the York Research Corpora-
     tion Monitoring trailer and was injected at specifically
     controlled rates from the master control panel located
     within the trailer proper.

     In addition to the standard calibration methodology, the
     calibration gas was injected up an auxiliary sample
     carrying line into the probe and then returned to the
     analyzers through the  usual passageways.  Utilizing this
     method, York engineers could determine if probe or sample
     line leakage existed.

     As a final check on the instruments, York Research per-
     formed wet chemical testing under strict EPA guidelines.
     Samples were taken simultaneously at the inlet position
     and the trailer's analyzer lead-in, and then again at the
     outlet position and the trailer's analyzer lead-in.  The
     following methods were used to verify instrumentation:
          •  Sulfur Dioxide:  EPA Method #6
          •  Nitrogen Oxide:  EPA Method #7
          •  Carbon Dioxide, Oxygen, and Carbon Monoxide:
             EPA Method #3.
                            -19-

-------
      TABLE 4-2.   VALIDATION OF INSTRUMENTAL DATA

Parameter (Location)
so2
so2
°2
°2
co2
co2
(Enlet)
(Outlet)
(Inlet)
(Outlet)
Clnlet)
(Outlet)
No. of
Tests
10
13
2
1
2
1
Avg. Concentration
Manual
1028.
490.
6.
6.
13.
11.
8 ppm
3 ppm
3 %
4 %
0 %
6 %
Instrumental
1035.
488.
6.
6.
13.
12.
0 ppm
7 ppm
4 %
8 %
1 %
7 %

4.1.5  Operational Data
     In addition to the test programs described, consider-
     able attention was paid to the acquiring of operational
     data for the boiler, the electrostatic precipitator,  and
     the scrubber.  Logs similar to those compiled in the con-
     trol rooms were kept by York Research personnel.  These
     data obtained include:
              •  Boiler Load (MW)
              •  Steam Temperature
              •  Superheater Temperature
              •  Reheater Temperature
              •  Pulverizer Mill Outlet Flow
              •  Pulverizer Mill Temperature
              •  Burner Tilt Position
              •  Combustion Air Temperature
              •  Coal Feed Rate
              •  Supplemental Oil Rate
              •  Coal Composition


                 Notivication of malfunctions


                 Mist eliminator pressure drop

                            -20-
ESP
Scrubber

-------
               •  Dryer draft
               •  Outlet temperature
               •  Product temperature
               •  Absorber pressure drop
               •  Inlet temperature
               •  Slurry temperature
               •  Circulation rate
               •  Centrifuge feed rate
               •  MgO slurry feed
               •  Recycle pump speed
               •  Centrifuge torque
               •  MgO tank level
               •  pH
               •  S02 inlet
               •  S02 outlet
               •  Induction fan speed
     Each month a report was compiled containing the following:
               •  Statement of Program Progress
               •  Statement of Program Problems
               •  Discussion of data
               •  Raw emission data (Instrumental)
               •  Boiler operating parameters
               •  Scrubber operating parameters
               •  Chemical analysis of scrubber process streams
               •  Graphical representations of data and trends
               •  Daily log
     This information is summarized in Appendix B (Hourly Data).
     A Daily Log of the unit's operation as well as the monitor-
     ing program is presented in Appendix C.

4.2  FGD System Availability
     For the purposes of this evaluation, system availability
     has been defined as:
              Availability (%) = (tQ/t ) x 100
     Where:    t  = Total hours system operated
              t  = Total hours in test program
                            -21-

-------
     Based upon data taken from the operating logs,  the above
     relationship shows that the scrubber was available dur-
     inq approximately 48 percent of the test period.   Availa-
     bility includes all levels of operation; transient and
     steady-state alike.  It is estimated that of the  time the
     system was available, approximately 80 percent  of that
     was steady-state where the system was operating normally.

     There were several occasions in which one or the  other of
     the two stages was operating separately.  These are con-
     sidered to be transient conditions.  It should  be noted
     that a portion of the outage time was due to lack of
     MgO supplies, as well as the fact that MgO slurry feed
     pumps were inadequate for handling full flow.  The per-
     cent of availability then, could have been much higher
     had these deficiencies not existed.

4.3  Boiler and ESP Availability
     Oxygen and carbon dioxide levels were constantly  re-
     corded at the scrubber inlet as indicators of boiler
     operating status and/or leaks in the ductwork (which
     would affect SC>2 concentrations in the flue gas) .
     The levels of these two constituents remained very con-
     stant throughout the test program.  This was due  to the
     use of the excess G>2 monitor located in the plant control
     room which allowed operators to regulate the level of 02
     in the boiler within tight limits  (generally 3-4  percent)
     The boiler availability was good during the test  program.
     The boiler ran at varied loads due to changes in  demand
     or operation, but for most of the program it was  in the
     range of full load.

     The ESP also operated smoothly.  There are few  records
     in the operator's log of any ESP shut-down or upset
     during the test period.  All of the flue gas from Unit
     No. 3 passed through the ESP before entering the  first
     stage of the scrubber.  A duct to by-pass the ESP was
                              -22-

-------
constructed, but this feature was very rarely used
because very heavy grain loading was considered to be a
strain on the demonstration unit's hardware.   This type
of operation was restricted to a few demonstrations.
                      -23-

-------
-24-

-------
5.0  TEST RESULTS
     5.1  Boiler and ESP
          The scrubber was designed to perform under a variety of
          boiler operating levels,  and in practice it did this
          well.  Unit No. 3 had a good performance record.  Table
          5-1 presents the operating parameters of the boiler.

     5.2  Scrubber:  Steady-State Operation
          During the test program,  the scrubber handled greater
          than 100 percent of the design flow on several occasions,
          but for the most part it ranged between 50 percent and
          90 percent of its design capacity.   On occasions when the
          boiler load was reduced because of  wet coal or a loss of
          coal feeders, the scrubber seemingly operated independ-
          ently of this reduction.   The only  effect was a drop in
          the S02 inlet concentration of approximately 200 ppm (or
          15 percent).  The second stage slurry pH values rose
          slowly in this case, and the MgO feed rate was lessened
          to compensate.  Otherwise, this drop in load would not
          notably effect the scrubber.

          The particle removal efficiency of  the scrubber with-
          out the ESP preceeding it ranged between 99.2-99.7 percent.
          With the ESP in line, the scrubber's particle removal
          efficiency was between 94.1-99.5 percent.

     5.2.1  Scrubber First Stage
          Flue gas entered the first stage from the air preheater.
          Table 5-2 lists the ranges for the  operation and chemical
          analyses performed on this stage.
                                 -25-

-------
              TABLE 5-1.  BOILER OPERATING PARAMETERS
                 Parameter
  Range
 Average
Load MW (gross)



Average Capacity Factor



Burner ^ilt  (degrees off vertical)



Super heciter Steam Flow  ( Ubs/hr)



Flue Gas; Temperature  (°F)



Flue Gas; Flow Rate  (ACFM) (full load)



Excess Oxygen  (%)



Combustion Air Temperature  (°F)



Coal Consumption  (tons/hr)



Heat Input ( 10   Btu/hr)



Coal Composition



Heat Cor.tent  (Btu/hr)



Sulfur (%)



Carbon (%)



Nitrogen  (%)



Oxygen (%)



Hydrogen  (%)



Ash  (%)



Moisture  (%)



Flue Gas Composition  (inlet to scrubber)
88-190
+12 to -8
3-4



510-585
10,100-12,600




1.20-3.30



59.0-72.90




0.87-1.50



2.7-9.50




3.4-4.8



13.8-21.7



0.4-2.5
Oxygen  (%)



Carbon Dioxide  (%)



Nitrogen Oxides  (ppm)



Sulfur Dioxide  (ppm)



Moisture  (%)



Grain Loading  (ESP on)(gr/SCF)



Grain Loading  (ESP off)(gr/SCF)



Duct Temperature  (°F)
5.0-10.0



11.0-17.0



340-520



660-1680



5.1-8.7



0.09-0.25



2.60-4.40
81








1,300,000




259




590,000
74.5




1744








11,000



1.74



66.6




1.30



5.35




3.89



17.2




1.3
0.3



3.0




240
                                -26-

-------
TABLE 5-2. SCRUBBER FIRST STAGE OPERATING PAKAMF.TKRS
                Parameter
Minimum  Maximum  Avg,
Inlet Gas Temperature  (°F)
Inlet Gas Flow (ACFM)
First Stage Pressure Drop  (inches 1^0)
Mist Eliminator Pressure  (inches 1^0)
Recycle Rate  (gpm)
Bleed Rate (gpm)
Compositions
First Stage Bleed
  PH
  Suspended Solids  (mg/1)
  Magnesium (mg/1)
  Chloride (mg/1)
  Sulfite (mg/1)
  Sulfate (mg/1)
Thickener Overflow
  Recycle Line (gpm)
  Suspended Solids  (mg/1)
  Suspended Solids Removal Efficiency(%)
  PH
  Chloride (mg/1)
Thickener Underflow
  Suspended Solids  (mg/1)
  Suspended Solids Removal Efficiency(%)
  PH
  Chloride (mg/1)
  250     265
  100,000 300,000
  11.4    12.5
  0.1     1.3
  2850    3100
  1.1
  0.5
  11.8
  7.5
  0.1
  35.0
6.1
966
113.9
2550
0.5
4340
*0.5
8.2
1.1
7.5
<0.5
1.6
1.3
11.0
317
83.9
6.4
2550
376
93.0
6.3
2550
                  980
                  20
                                -27-

-------
TABLE 5-2.  SCRUBBER FIRST STAGE OPERATING PARAMETERS  (CONT.)	

                  Parameter                   Minimum   Maximum  Avg,

Particle; Removal Efficiency
  With E,SP in line  (%)                           94.1       99.5
  Without ESP in line  (%)                        99.2       99.7
Sulfur Oxides Removal Efficiencies  (%)            5.0       10.0
                                -28-

-------
5.2.2  First Stage Bleed
     The first stage bleed was the liquid sent to the
     thickeners for clarification after being circulated
     through the venturi throat along with the flue gas
     and had impacted the solid particulate matter.  The
     samples were collected at the distribution box where
     the liquid from the bleed line was separated.  The
     parameters determined were chosen to characterize
     the first stage recycle liquid for corrosiveness and
     to determine the amount of spill-over from the second
     stage absorber.

     A pH as high as 6.1 occurred when a very light gas flow
     passed through the inlet.  The pH always dropped with
     the length of time the scrubber was in operation be-
     cause of the formation of acids (sulfuric, sulfurous,
     hydrochloric and some nitric from the absorption of
     gases in the water).  An equilibrium pH value of 1.1-
     1.4 was reached after the longest run for which these
     data were obtained  (84% hours).

     In order to determine if there was any cross-over con-
     tamination from the second stage's scrubbing water to
     that of the first, testing was performed to determine
     the magnesium ion (Mg  ) concentrations in the first
     stage.  The Mg   levels in the first stage bleed ranged
     between 11.8-113.9 mg/1.  Contributors could have been
     the make-up water, the flyash, or contamination from
     the second stage.  It seems that the make-UD water
     was the most likelv source of Mg   in view of the
     magnitude of the maximum (113.9 mg/1).  When tested in
     August 1974, the make-up water indicated levels of Mg
     ranging between 71.0-102.6 mg/1.  Any reasonable increase
     in the Mg   concentration over these values could be
     attributed to the recycling of the process water through
     the first stage.
                            -29-

-------
The suspended solids level in this bleed line was a
measure of thickener efficiency.  Naturally, the level
was low shortly after start-up, but rose to a high of
nearly 1000 mg/1 as operation was continued.  As the
thickener achieved an equilibrium operating state, the
suspended solids level would drop from this maximum.

The presence of chloride and its associated corrosion
problems was also investigated.  The chloride ion
concentrations were generally quite high, because the
liquid was recycled, and the levels would increase as
scrubber operating time increased.

The coal tested during a baseline study showed a
chloride content of between 0.03-0.14 percent.  Un-
doubtedly this was the primary origin of this ion in. this
first stacre recycle bleed liauid, as it was absorbed
from the flue eras or flyash,  It is unlikely that
this chloride level could have been introduced from the
river water used for make-up because other parameters
which were measured in this make-up water were very
low.  The iron, sodium, copper, mercury, phosphate and
fluoride, when tested earlier were present in quantities
low enough for the river water to be considered a re-
latively non-polluted surface water.  The resulting cor-
rosiveness could have been responsible for the occurrence
of leaks in the first stage piping.  Sections 6.0 and 7.0,
and Appendix F describe these in detail.

The levels of SO^ (sulfite) and SO^ (sulfate) were
approximately those which would be expected.  They
originated from the minimal absorption of sulfur oxides
from the flue gas into the first stage liquid.  Previous
testing had shown that the concentration of SO., in the
flue gas ranged between 0 and 55 ppm.  SO^ levels averaged
about 1000 ppm in the stack gas.  The first stage of the
scrubber normally removed between 5 and 10 percent of the
SOj in the flue gas, which formed sulfuric acid as it

                       -30-

-------
     dissolved in the liquid.   The highest level of S04 measured
     was 3738 mg/1 which is equivalent to a 0.1 normal sulfuric
     acid solution.

     Thus the corrosive nature of this recycling bleed was
     established, and was considered to be sufficiently
     high to breakdown even No. 316 stainless steel.  (R.  Glenn,
     Weekly Technical Report,  January 27, 1975).

5.2.3  Thickener Overflow
     The thickener overflow was the clarified water from the
     thickener tanks.  After being mixed with make-up
     water, this overflow was returned to the scrubber first
     stage.  Make-up water was added to the system to replace
     that portion of the liquid going into the thickener under-
     flow, and that lost due to evaporation.

     Testing of this stream was done to determine the levels
     of suspended solids, chloride ion, and pH.  The suspended
     solids remained in a range which indicated an adequate
     performance of solids removal by the thickener system.
     When the first stage recycling system reached equili-
     brium, the solids in the overflow ranged between 20-80
     percent of the suspended solids level in the bleed line.
     The pH and chloride ion levels paralleled those of the
     first stage bleed as these concentrations were unaffected
     by the addition of flocculant to the liquid, or settling.

5.2.4  Thickener Underflow
     This stream was the slurry product of the thickener
     flocculation process.  The slurry was pumped to a transfer
     tank, and thence to a series of settling ponds.  The
     water from the settling ponds was subsequently used to
     dilute the thickener underflow slurry in the trans-
     fer tank.  Suspended solids, chloride ion levels, and pH
     were generally similar to those of the overflow samples.
     The efficiency of the thickener was minimal at low solids
                            -31-

-------
     concentrations (1.6 percent);  however,  it increased to a
     high of 93.0 percent removal when the incoming slurry
     (first stage bleed) had a high suspended solids content.

     More definitive observations could have been made if the
     duration of periods of scrubber operation had been longer
     during this study of the first stage.  Chloride concentra-
     tions were still climbing when the scrubber shut down due
     to a build up of product in the dryer.   Other trends in
     solids removal may have become more evident during a longer
     operating period.

5.2,,5  Scrubber Second Stage
     After passing through the mist eliminators the gas was
     processed in the MgO absorber of the second stage.  The
     dryer off-gas was also scrubbed in this section to re-
     move any sulfur oxides and other pollutants generated from
     the oil combusted to heat the dryer.  Table 5-3 lists the
     operating ranges of the various parts of this stage.
                            -32-

-------
TABLE 5-3. SCRUBBER SECOND STAGE OPERATING PARAMETERS.
Parameter
Inlet Gas Temperature (°F)
MgO Storage Silo capacity (tons)
MgO Belt feed rate (#/min)
% MgO
% MgS04
MgO Slurry feed rate (gpm)
MgO Slurry temperature (°F)
Pressure Drop total (inches H20)
-absorber (inches H20)
-mist eliminator (inches H20)
Absorber circulation rate (gpm)
Second Stage Bleed rate (gpm)
Second Stage Bleed Composition
PH
MgS03'6H20 (%)
Suspended Solids (%)
SO| (filtrate) (%)
MgO in solids (%)
Density (g/ml)
Outlet Gas Flow (ACFM) *
Outlet Gas Composition
Particulate (gr/SCF @ 12% C02)
02 (%)
C02 (%)
Minimum
110

15
85.0
0.01
6
120
0.4
0.4
0.1
4600


5.5
0.07
0.16
0.5
0.06
0.99
81,800

0.0009
5.0
10.4
Maximum Average
120
100
25
96.2 90.1
12.57 2.75
25
165
13.0
4.0
1.0
5500
170

8.0
11.74
19.79
22.1
41.86
1.34
159,000

0.020
10.0
16.0
*Includes dryer off gas flow, which is added into Second Stage
                                -33-

-------
TABLE 5-3. SCRUBBER SECOND STAGE OPERATING  PARAMETERS  (CONT.)
Parameter
S02 (ppm)
NOX (ppm)
Moisture (%)
Outlet temperature (°F)
S02 Removal Efficiency (%)
Centrifuge feed rate (gpm)
Centrifuge Cake Composition
Density (g/ml)
Combined Water (%)
Free Water (%)
MgS03 (%)
MgS04 (%)
MgO (%)
Mother Liquor Composition
Solids (%)
MgS03'6H2O (%)
MgO (% in solids)
MgO (% total)
Density (g/ml)
Dryer Outlet temperature (°F)
Dryer Product composition
Water (%)
MgS03 (%)
Minimum
63
320
7.5
111
61.0
90

1.00
42.0
7.0
40.0
3.0
0.75

0.08
0.16
0.20
0.01
1.01
200

0.2
60.0
Maximum Average
350
450
13.0
145
93.0
132

1.60
47.0
15.0
45.0
6.0
7.0

12.62
11.58
21.96
4.05
1.34
450

15.0
75.0
                                -34-

-------
TABLE 5-3.  SCRUBBER SECOND STAGE OPERATING PARAMETERS (CONT.)

Parameter
Dryer Product Composition (Cont.)
MgS04 (%)
MgO (%)
Density (g/ml)
MgS03 Silo Storage capacity (tons)
Minimum

5.0
2.0
0.45

Maximum

10.0
10.0
0.70

Average




200
     5.2.6  The MgO slurry was prepared by mixing a weighed amount
          of MgO from the storage silo with the mother liquor from
          the centrifuge.  The weigh feeder belt delivered between
          15 and 25 Ib./min. of MgO.  The accuracy of this belt was
          not as dependable as was expected.  This made the addition
          of MgO slurry into the scrubber difficult and caused a pro-
          blem for the operators who were attempting to regulate the
          pH by this method.

          During October, 1974, 200 tons of MgO were used.  This
          was a mixture of virgin and regenerated MgO in a ratio
          of approximately 1.5:1.  In November, 73 tons of additional
          virgin MgO were added to the silo.  The rest of that month
          the scrubber operated using regenerated MgO.  Later in
          December and January, some small quantities of virgin MgO
          were added to the silo to replenish the MgO that was lost
          in operation and in transportation.

          Throughout the test program, the MgO was analyzed for
          MgS04 and MgO content.  The samples ranged between 85.0-
          96.2 percent MgO and 0.01-12.57 percent MgSO4-

          The amount of MgO indicated the purity of the product used.
          No specific analyses for impurities were performed by York
          Research chemists, however, so the percent difference be-
          tween the total of the percent MgO and percent MgSO. from
                                   -35-

-------
     100 percent was assumed to provide the amount of foreign
     material present.   These impurities could have originated
     from the flyash which was carried through the system into
     the second stage,  or from corrosion and/or erosion pro-
     ducts in the scrubber itself.   Since this product was
     effectively recycled, these impurities increased with
     each absorption-recalcination cycle.  Ultimately, these
     impurities could have reduced the reactivity of the MgO
     so as to render it useless.

     The MgO slurry was mixed with the mother liquor and
     heated by a steam sparger.  The slurry was then pumped into
     the second stage nozzles above the venturi.  The stack gas
     and the MgO slurry proceeded through the venturi together.
     The scrubbed gas flowed through the mist eliminators to
     the scrubber outlet and the stack.  The slurry dropped to
     the bottom of the second stage and was recycled through
     this process.

5.2.7  Second Stage Bleed
     A small portion of the slurry containing unreacted MgO
     and the product MgSO^ was bled off at a rate of 120 gpm
     and processed in the centrifuge.  Make-up water was
     added to the absorber to maintain the proper consistency
     of the slurry.  Fresh MgO slurry was added at a rate reg-
     ulated  by the operator to adjust pH.  An ideal pH was
     between 6.8-7.2, because this range maximized the SO2 ab-
     sorption process without producing a build-up of crystals
     in the absorber.  This also assisted the centrifuge and
     dryer to attain optimum performance. However, due to the
     difficulty in regulating the pH by MgO addition, normal
     operation included pH values ranging from 5.5 to greater
     than 8.0.

     The lower pH values were indicative of problems that
     developed in the MgO slurry feed or recycle systems.
     These problems had the effect of reducing the amount
                              -36-

-------
of MgO being pumped into the scrubber to a level that was
lower than that required to react with most of the S02
present.  The presence of excess S02 increased the acidity
of the slurry.  When the pH was allowed to drop below 6.8,
corrosion of ductwork and piping could have become acute.
The higher values occurred shortly after the scrubber
startup, before the S02 in the stack gas had been thoroughly
mixed with the absorbent MgO slurry.  At this time the pH
was as high as 9.4.

The solids content of this bleed slurry ranged between
0.16-19.79 percent.  The different levels were due to
changes in the MgO slurry feed rates, and the variations
in flue gas flow into the scrubber.  Both of these rates
were manually set by the scrubber operators.  The low values
represented the initial operation shortly after the start
up when the scrubber operated with reduced gas flow from
the boiler.  Values ranging from 3-8 percent were typical
of favorable MgO feed rates and a proper pH level in the
absorber slurry.  Solids above 18 percent were not de-
sirable because the pumping system from the absorber to
the centrifuge could not adequately handle the crystals
in the absorber slurry which forced the gas load to be
reduced until the crystals could be freed.

The composition of these solids was studied to determine
the amount of product  (MgSO.,) formed in the absorber.
Naturally, the higher this percentage, the more efficient
the operation.  The range for the test program was 0.07-
11.74 percent MgSO.,.  Another component of the solid
portion of this slurry was MgO (range 0.09-19.6 percent).
The difference was composed of impurities and insoluble
sulfates.

The slurry density was also measured.  This measurement
gave a rough indication of the type of slurry that was
introduced to the centrifuge.  Operational changes could
have been made using this parameter to obtain a more con-

                       -37-

-------
     sistent product and reduced wear on the system.

5.2,,8  Centrifuge Cake
     The slurry was introduced to the centrifuge to separate
     the solid and liquid portions.  The centrifuge cake
     (solid portion) was analyzed to determine the character
     of the product.  The bulk density was measured to in-
     dicate the free water in the cake.  As the percent water
     increased the density decreased/ which meant that the
     centrifuge efficiency had decreased.  A very wet cake
     put a strain on the screw conveyor and dryer.

     During August, the amount of free water was as high as
     29.8 percent.  The chemical analysis of the cake was
     comparable to past cakes; therefore, the cause of the
     high water content was possibly due to centrifuge per-
     formance.  The centrifuge weir heights, which controlled
     the degree of liquid/solid separation, were adjusted dur-
     ing the August 26, 1975 outage but no chemical analyses
     were performed after this date to determine if the cent-
     rifuge was the problem.

     The percent MgO was measured to determine the amount of
     unused reactant leaving the absorber.  Low MgO concen-
     trations (less than 3 percent) reflected good absorption
     in the second stage.  High values (above 6 percent) re-
     flected a high pH in the absorber, low gas flow, low
     reactivity of the MgO, or decreased slaking due to fail-
     ure of the steam lines to the MgO slurry make-up tank at
     certain times.

5.2.9  Mother Liquor
     The liquid separated by the centrifuge was returned to
     the process to be recycled.  Most of it was pumped
     directly into the second stage of the scrubber below
     the venturi.  A small portion was used with the MgO
     to make up the MgO slurry.
                           -38-

-------
     The solids concentration in this liquor varied inversely
     with the efficiency of the centrifuge.   A determination
     of the reacted product MgSCU was made to observe the amount
     that was recycled.   The percent MgO was also monitored.
     High MgO readings may have resulted from a high second
     stage pH, unreactive MgO, or decreased slaking in the
     MgO slurry tank.

5.2.10  Dryer Product
     The dryer prepared the centrifuge cake for storage and
     shipment to the calcination facility.  Final composition
     analyses were performed on this product.  Water content
     ranged between 0.2-15.0 percent.  MgSO^ content was nor-
     mally within 60-75 percent and the unreacted MgO levels
     were between 2.0-10.0 percent.

     The percent MgO in the dryer product was analyzed in
     order to determine how much unreacted material was
     being carried through the system and being shipped out for
     regeneration.  A low percent MgO reading was desirable
     because it reflected good S02 absorption and economical
     operation of the system.  Among the factors that may have
     effected high MgO readings are a high pH in the second
     stage slurry, unreactive MgO, and decreased slaking due
     to failure of steam lines to the MgO make-up tank.  Varia-
     tions in MgO content could be attributed to pH fluctuations
     in the absorber, changes in the volume of flue gas pro-
     cessed, the type of coal burned, the percent of MgO in
     the slurry, and centrifuge efficiency.

     The bulk density of the dryer product was measured as an
     indication of the character of the product.  This would
     have been an aid in determining the volumes and weights
     of the product for shipment and bucket elevator performance,

     In January 1975, a high percentage of 1^0 in the dryer
     product was deliberately induced in order to determine
     the effect of percent H~0 on the bulk density.  It was
                           -39-

-------
     found that increased in I^O did increase the bulk density.
     This was significant because shipping and handling costs
     could definitely be affected by the moisture content of
     the dryer product.

     A question was raised regarding the iron content of the
     system.   All of the existing pipes leading from the
     second stage back to the dryer system were composed of
     carbon steel.  After a lengthy outage, October 26 to
     November 10, 1974,  the iron content of the system was
     measured by analysis on the dryer product solids at two-
     hour intervals.  Upon start-up, the iron in the first dryer
     product sample was determined to be 3.77 percent Fe203.
     Within a twentyfour-hour running period, the iron content
     diminished to the 200 ppm (0.2%).Fe203 and held constant
     at that level for a sustained period. .The results are
     plotted in Figure 5-1.

     Chloride concentration in the coal was found to be 0.02-
     0.20 percent at this time.  (Chlorine from the coal com-
     bustion forms HCl gas which reacts with the MgO (aq.)
     forming soluble MgCl2«  It was believed that the Cl'tMgC^)
     concentration continually increased with on-line time
     since the soluble MgCl2 was circulated through the system
     continually via the mother liquor.

5.3  Scrubber:  Transient Operation
     Transient operation occurred during scrubber start-ups,
     shut-downs and malfunctions.  The major point of interest
     in the documentation of these conditions was their effect
     on emissions.

5.3.1  Start-Ups
     Before starting the scrubber induced draft fan (ID), it
     was necessary to prepare the scrubber to receive stack
     gas.  The MgO slurry for use in the second stage of the
                           -40-

-------
O
CM

0)
z
w
w
       00
02
04
06
08
16
      10     12    14



        TIME OF DAY



DRYER PRODUCT Fe203  (11/10/74)



         FIGURE 5-1
18
                                                                      20
                                                                22

-------
     scrubber was mixed in the slurry make-up tank.   This
     slurry was then pumped in and circulated through the second
     stage.  First stage liquid,  which was a combination of
     the thickener overflow liquid and make-up water, was also
     circulated through the scrubber.  As the scrubber ID fan
     was started, dampers on the inlet and outlet to the scrub-
     ber were opened, allowing the stack gas to circulate.
     When a sufficient amount of MgS03 crystals had formed in
     the second stage, the centrifuge, dryer, and solids hand-
     ling equipment were placed in service.

     Within a few minutes the SO- removal efficiency was typi-
     cally 70-80 percent.  Additional information on S02 con-
     centration and percent SC^ removal during several start-
     ups is included in Appendix E.

5.3.2  Shut-Downs
     Prior to stopping gas flow to the scrubber, SOj removal
     efficiencies were observed between 70-80 percent.  Table
     5-4 shows typical shutdown data.  More detailed informa-
     tion is presented in Appendix E.

5.3.3  Malfunctions
     Table 5-5 summarizes the overall effect of several major
     transient conditions.  Generally, if equipment failure
     caused shutdown of major components such as the centri-
     fuge, or required major changes in liquid or gas flows,
     then SO- removal was significantly reduced.

     Generally, many of the malfunctions, and the leaks dis-
     cussed in the following Section, were attributable to the
     delivery of off-specification pipe and fittings during
     construction, and to the use of off-specification nuts,
     bolts, hanger rods, and nozzles.  In addition, in some
     cases, stainless steel was of an improper grade, and
     rubber linings were too thin and poorly bonded.
                           -42-

-------
TABLE 5-4. PERCENT S02 REMOVAL AT SHUTDOWN.

Boiler
Load
Date Time (MW)
11/11/74 0145
0200
0215
0230
0245
11/16/74 2045
2100
2115
2135
i 2145
*>.
CJ
' 0800 140
12/23/74 0900 169
0930
1900 188
1915
11/12/75 1930
1945
2000 185
0730
0745
11/24/75 0800 147
0815
0830
0845
Scrubber Ap
2nd Stage
(in. H20 }

1.0

0.0




0.0



8.0
6.2
—





4.9
6.8
5.5
6.4
0.0

Inlet
Scrubber SO 2
pH (ppm)
6.0
1175

5.6 1200


7.4 1000

1000



7.0 880
7.2 860
— —
7.1
920

900
7.0
900

7.3 900

850

Outlet S02 Removal
S02 Efficiency
(ppm) U)
220

250

1200
210

210

1000


160
160
—
185

150

OFF SCALE

190

190

850
78.0

78.7

0.0
79.0

79.0

0.0


81.8
81.4
0.0

80.2

83.3


78.9

78.9

0.0

-------
                                       TABLE 5-5.   SUMUIRY OF MAJOR TRANSIENT CONDITIONS
Condition
Centrifuge Repair - Cover
leak erosion of carbon
steel

Centrifuge Diversion-Main-
tenance procedure - wash
out the chute

Centrifuge Diversion -
Clogged hopper-wet centrifuge
cake, possibly due to im-
proper weir height

1st Stage Outage - Leak - 1st
Stage recycle lines. Breaks
in rubber lining exposed
carbon steel pipe to low pH/
high abrasive content liquid
of 1st Stage


2nd Stage Outage - Leak in
discharge header-abrasive
action of the solids laden
slurry
2nd Stage outage-Repair re-
cycle header-20" pipe very
thin due to abrasive action*
holes easily formed
2nd Std<,e Outage

Time of
Transient
Condition

11/15
1000-1500

0430-0515
1/14




0100-0145
12/28





1200-1250
12/7




1300-1400
12/16


1000-1200
12/19
1900-2000
8/26
Transient Previous* Transient
Previous* Transient Previous* Condition % SO? Condition
2nd Stage Condition SO2 Out- SO 2 Outlet Removal * SO?
Ap Ap let(ppm) (ppm) Eff. Removal Eff


8.0 4.1 125 175 85.6 75.9

NA NA 160 160 84.0 84.3






NA NA SO 70 90.9 91.9






9.3 3.0 169 230 80.9 74.2





6.2 0.0 168 683 82.2 23.1



8.4 NA 206 300 82.1 75. 0
3.4 0.8 302 1075 73.2 4.4



Slurry feed
flow rate
had to be
reduced and
scrubber
init could
not handle
design gas
flow. Un
treated por-
tion was by
passed to
stack



Scrubber
unit could
not handle
design flow.
Untreated
portion was
bypassed to
stack






* Refers to steady-state conditions  in  existence prior  to  the transient condition.

-------
                                                 TABLE  5-5.  SUMMARY OF  MAJOR TRANSIENT CONDITIONS (COMT) .
U1
 I
Condition
Boiler load was reduced-
Wet coal-high surface
moisture reduced pulver-
ized mill outlet temper-
atures to below the ISOop
minimum needed to maintain
an adequate drying cake.

Rising Boiler Load -
Partial alleviation of
wet coal problem

Coal feed problem required
reduced boiler load - Wet
coal - agglomeration of
coal particles before the
pulverizer
Tine of
Transient
Condition





1500-0800
12/8-12/9


0900-2400
12/9




2200-2000
12/20-12/21
Transient Previous *
Previous* Transient Previous* Condition % SOj
2nd 'Stage Condition SC>2 Out- SC>2 Outlet Removal
Ap Ap let(ppm) (pptn) Ef f .





8.5 4.1 143 273 85.4




4.1 5.4 273 207 75.3





6.2 3.6 232 232 81.7
Transient
Condition
« SO,
Removal Eff





75.3




77.6





78.2





Gas flow
through the
scrubber was
reduced and
SO 2 emissions
were used
under the
period .





                 Refers  to  steady-state  conditions in existence prior to the transient condition.

-------
     The scrubber's absorption efficiency was not unusually
     sensitive to gas flow because the venturi design provided
     greater than 70 percent of S02 removal even though Ap
     was reduced by 50 percent and gas flow was 70 percent of
     the normal rate.

5.3.4  Leaks
     Table 5-6 details the frequency with which individual
     leaks occurred.  Apparently there were twice as many
     leaks causing shutdown in the first stage of the scrubber
     as in the second stage.  The rubber-lined pipes in the
     first stage sustained more mechanical damage because
     they were subjected to extraneous material (such as
     pieces of weld), which might have been carried in
     with the flue gas.  In addition, extensive corrosion
     and erosion were noted from tests performed.  Both
     chemical and visual observations to this affect were
     performed.

5.3.5  Centrifuge Outages
     Approximately 1.6 percent of the total recycle of the
     second stage was taken from the discharge of the recycle
     pumps to the centrifuge.  The centrifuge normally re-
     moved 50 percent of the solids in this liquid stream.
     During the course of the scrubber study, the centrifuge
     had to be diverted numerous times because of clogging
     or leaks that developed in its cover.  Consequently, no
     solids were removed during these periods.
                           -46-

-------
                             TABLE 5-6.

               LEAKS NOV.,  DEC.  '74;  JAN.,  AUG.  '75

Affected Component
First stage bleed line
First stage recycle lines
First stage headers
"A" 1st stage pump
Reducer, Nozzle lines, and pump
Second stage bleed lines
Second stage recycle line
Second stage discharge headers
Second stage drain connection
"B" discharge pump
Centrifuge Cover
Occurrences
7
9
6
2
4
1
2
5
1
1
9
Number
Inducing
Shutdown
3
4
1
2

1
1
1
1
1
1
Duration
of
Outage
150 hrs.
153*
41 hrs.
h hr.

66 hrs.
28 hrs.
2J$ hrs.
81 hrs.
2 hrs.

*  This excludes a 14 day outage begun August 27, 1975 to replace
   the lines.
                                 -47-

-------
         The effect of a typical centrifuge malfunction requiring

         shutdown for repair is summarized below:
                   TABLE 5-7.  CENTRIFUGE REPAIR
Condition
Second Stage
AP       PH
  S02 Outlet
Concentration
     (ppm)  .
SO-, Removal
Efficiency
Steady-S4:ate
Condition Before
the Centrifuge
Repair
(0400-0900,11/15)

Centrifuge Repair
(1000-1500,11/15)
 8.0
 4.1
7.5


7.0
      125
      275
    85.6


    75.9
         Centrifuge shutdown occurred at 0940.  To prevent build-

         up of excess solids, gas flow to the unit was reduced at

         1000.  It was further reduced at 1030 when no progress

         was made on the repair.  The second stageAp had been

         8.0 inches of water.  As a result of the reduced gas

         flow and Ap of 4 inches, S02 removal efficiency dropped

         from 85.6% to 75.0%.  It eventually bottomed at 73.8%

         removal, but because of continued reduced gas flow, it

         did not stabilize until 1500 hours when the removal

         efficiency averaged 78.9%.
                                -48-

-------
Increased liquid/gas ratio somewhat off-set reduced gas
velocity through venturi yielding a somewhat lower S02
removal efficiency during the repair period.  The lower
pre-repair levels of S02 outlet emission were reached a
few hours later.  Lower gas flows were continued beyond
the return of the centrifuge to operation so a reduction
in the accumulated solids might be effected.  Excessive
solids build-up in the system placed undue strain on
pumps and increased erosion.  When a problem with the
centrifuge required a diversion, gas flow to the unit
was reduced before and during the Outage to reduce solids
build-up.

MgO slurry feed was reduced and the lessened gas flow
continued until accumulated solids had been separated
as shown below:

                TABLE 5-8.  CENTRIFUGE PERFORMANCE
Time
0800
1200
1600
Second Stage
Bleed (% Solids)
6.9
8.25
3.96
Mother Liquor
(% Solids)
1.16
3.99
1.33
The result of the 2-hour and 40 minute outage was a 5*s
hour period of higher than steady-state emissions.
Although stability was attained at the end of this time
period, emissions still had to fall to attain prior
steady-state levels.  It is concluded that continuous
reliable centrifuge separation of solids is important
to effective scrubber operation.
                       -49-

-------
     5.3.6  First Stage Outages
          A leak of the first stage recycle lines on December 7,
          1974 necessitated a complete first stage shutdown.  The
          first stage was down for 50 minutes, from 1200 to 1250
          hours.  The effect is summarized in Table 5-9.

	TABLE 5-9.  FIRST STAGE OUTAGE	
                            Comparison of Parameters
                   Second Stage    S02 Outlet    % SO- Removal
    Condition	A P    pH	   (ppm)	Efficiency	
Steady-State Period
Prior to Outage
(0100-1000,12/7)      9.3   7.1        169           80.9
First Stage Outage
(1200-1250,12/7)      3.0   7.5        230           74.2
          Gas flow to the FGD unit was reduced and efficiency of
          SOo removal was reduced.  Additional data are presented
          in Appendix E.

     5o3.7  Second Stage Outages
          December 16, 1974 the second stage was shutdown at
          approximately 1255 to weld a leak in the discharge
          header.  As shown in Table 5-10, gas flow to the scrubber
          was reduced and the second stage Ap, which had been 6.4
          at 1200, dropped to zero.  Efficiency decreased from 83
          percent at 1200 to 23 percent at 1322, and stayed in the
          low 20's until start-up at 1510.  This Table compares
          the parameters from the steady-state period prior to the
          outage with those of the transient condition.
                                -50-

-------
                TABLE 5-10.  SECOND STAGE OUTAGE
Condition    Second Stage      SOj Outlet     % SO- Removal
              AP     PH    Concentration      Efficiency
	(ppm)	

Steady-State
Period Before
Outage (0500-
1200, 12/16)   6.2   7.2         168               82.2


Second Stage
Outage (1300-
1400, 12/16)   0.0   8.0         683               23.1
          This is typical of the efficiency reduction associated with
          a second stage outage.  Two other such outages occurred,
          and detailed data are presented in Appendix F.
                                -51-

-------
-52-

-------
6.0  ENGINEERING EVALUATION

Three primary goals can be outlined for the Magnesia FGD demon-
stration unit.  The first goal was to construct and operate the
system according to design specifications, for extended periods of
time.  The second goal was to study the sub-systems of the process
and optimize their performance in order to optimize the over-all
system performance.  The third goal was to vary the flue gas com-
position and flow rate to the system and observe the overall
system performance.  The following engineering evaluation of the
process is divided into these three sections.  The sections dis-
cuss (1) the operability of the process as it was designed,
(2) the optimization efforts undertaken, and (3) the over-all
performance of the system.

     6.1  Operability
          The operability of the system is discussed separately
          for the first and second scrubber stages along with their
          individual sub-systems.  These sections discuss the mal-
          functions, repairs, and maintenance performed during the
          test program.  Appendix F lists each malfunction and the
          type of maintenance performed in chronological order.
          These data were compiled from the Chemico Operator's Log
          and from the Weekly Technical Reports prepared by Mr.
          Roland Glenn.  The August 1975 listings in Appendix F are
          solely from Mr. Glenn's reports as no scrubber operator's
          log was available.

     6.1.1  Scrubber System First Stage
          Throughout the scrubber testing program, the system
          operation was hampered by malfunctions.  A majority of

                                -53-

-------
these malfunctions occurred in the first scrubbing stage
due to leaks in the pipes, valve liners, and headers.  The
areas most vulnerable to leaks were areas where the flue
gas changed direction within the scrubber or where rapid
slurry velocity increases occurred in piping such as at
elbows, reducers, and orifice plates.  Rubber liners in
the pipes and valves were torn and gouged by stray pieces
of metal in the system.  These breaks in the liner exposed
the steel pipe to the highly corrosive liquid of the first
stage.  Table 6-1 is a compilation of the leaks encountered
in the first and second stage during the periods of Novem-
ber and December, 1974, and January and August, 1975.

On January 18, 1975, after an inspection of the inside
of the first stage vessel, it was reported that six of
the ten tangential spray nozzles were missing.  The
probable cause of these stainless steel nozzle failures
was the high concentrations of chlorides, low pH of the
recycle slurry, and off-specification stainless steel.
Chloride from the combustion of the coal in the boiler
aided in the corrosion by pitting and etching the steel,
exposing surface area to sulfuric acid attack.  The pit-
ting was more prevalent on the outside of the nozzle
where acid mist had settled.  The use of acid resistant
coatings, rubber or plastic pipes and nozzles in this
location should be considered.

Available data indicate that leaks adversely affected
scrubber efficiency.when the repair undertaken.required
alterations in scrubber operating parameters.  A case in
point was provided by the data of December 7, 1974 when
a leak of the first stage discharge header caused the shut-
down of the entire first stage.
                        -54-

-------
             TABLE 6-1.  LEAKS OF THE SCRUBBER SYSTEM
             	Nov.,Dec.'74; Jan.,Aug.'75
  Scrubber Component
      Affected
Occurrences
 Number
Inducing
Shutdown
Emission Control
  Time Lost to
Outages (Approx.)
First Stage bleed line

First Stage recycle lines

First Stage discharge
headers

First Stage recycle
pumps

First Stage piping
     7

     9
   3

   4
   150 hrs.

   489 hrs.*


    41 hrs.


     % hr.
reducers and nozzles
Second Stage bleed lines
Second Stage recycle line
Second Stage discharge
headers
Second Stage drain
connection
Second Stage recycle
pumps
Centrifuge cover
4
1
2
5
1
1
9

1
1
1
1
1
1

66 hrs.
28 hrs.
2*s hrs.
81 hrs.
2 hrs.


* This includes a 14 day outage begun August 27, 1975 to replace
  the lines.
                               -55-

-------
          On this occasion,  the first stage was down for 50 minutes,
          from 1200 to 1250  hours.   The short duration permitted
          but one set of wet test readings for the outage which
          appear in Table 6-2.  Also included are the average
          parameters for the steady-state period immediately before.
          The drop in efficiency induced by the first stage shut-
          down was approximately 7 percent.  S(>2 outlet concentra-
          tions increased by 36 percent.  Scrubber operators re-
          duced inlet flows  during the outage and the second stage
          pressure drop decreased.   This, in turn, contributed to
          reduced performance.  The pH was also affected by the
          lower gas flows.  In this case it was a combination of
          lower flows and insufficient reduction in the MgO slurry
          feed rate that led to a higher pH reading.

          Inspection of the  demister in the first stage indicated
                 TABLE 6-2.  FIRST STAGE OUTAGE
                              December 7, 1974
Condition
Inlet
Plow
ACFM*
Comparison of Parameters
% so2
Second Stage S02 Outlet Removal
Ap pH (ppm) Efficiency
Steady-State
Period Prior
to Outage
(0100-1000,12/7)  230,000  9.3    7.1      169           80.9
First Stage
Outage
(1200-125D,12/7)  140,800  3.0    7.5      230           74.2
* At the inlet to the first scrubber stage.

          that there was no problem with solids deposit formation.
          The principal problem with the demisters appeared to be
          from physical abuse from being walked on during in-
          spections.  There was no apparent reduction, however, in
          the performance of this equipment.

                                -56-

-------
6.1.2  Solids Removal Section for the First Stage
     Generally, there were few problems in the operation of
     the solids removal section of the first scrubber stage.
     This can be attributed to two operating conditions that
     existed during the test period.   The first was the flue
     gas which came directly from the electrostatic precipi-
     tator the majority of the time.   As a result there was not
     a very heavy load placed upon the solids removal equipment.
     The second condition that existed were dual particle
     removal systems which allowed each thickener to operate
     independently of the other.  Consequently, there was only
     one instance where the solids removal equipment forced a
     shutdown of the scrubber system.  This occurred on Janu-
     ary 19, 1975 and was the result of a restriction in the
     first stage bleed line.

     The thickener overflow and underflow were not sampled
     on a routine basis until August 1975.  During August, the
     longest sustained operating period was 85.5 hours.  Since
     complete test data are lacking,  nothing more can be said
     about the operability of this section other than to note
     the few failures which occurred in the list of scrubber
     malfunctions in Appendix F.

6.1.3  Scrubber System Second Stage
     Malfunctions in the absorber section of the second stage
     were not as numerous as those in the first stage where the
     pH was very low.  Leaks in the second stage recirculation
     piping were caused by abrasion,  where the solids in the
     slurry  eroded and finally destroyed the piping.  From
     thickness measurements made by Chemico personnel with an
     ultrasonic thickness measurement instrument on the second
     stage lines, the pipes showed excessive erosion on sur-
     faces where maximum abrasion would be expected.  These
     areas were primarily the elbows, reducers, and places
     where a change in flow direction occurred.  The MgO
     slurry contained up to ten percent solids under normal
     operating conditions.  This accounts for the abrasiveness
                            -57-

-------
of the slurry, especially on unlined steel piping.
Decreases in liquid velocities slowed this wear, but
installing abrasion resistant rubber liners would have
been more desirable.

There were three second stage outages during the scrubber
study:  December 16, 1974, December 19, 1974, and August
26, 1975.  On December 16, 1974 the second stage was shut
down at approximately 1255 to weld a leak in the discharge
header.  (The first stage was still operational).  Scrubber
inlet gas flow was reduced and second stage  Ap, which had
been 6.4" H20 at 1200, dropped to zero.  Efficiency de-
creased from 83 percent at 1322, and stayed in the low
20's range until startup at 1510.  Table 6-3 compares
the parameters from the steady-state period prior to
the outage with those of the transient condition itself.
The steady-state period was from 0500 to 1200 hours on
12/16.

During this outage the S02 removal efficiency remained
at approximately 20 percent for an hour and 45 minutes
after the second stage was off-line.  Apparently, the
MgO slurry remaining in the absorber without being cir-
culated absorbed a small amount of S02 until the surface
became saturated.  Normally, the first stage removed be-
tween 5-10 percent of the S02 in the flue gas.  This was
measured when the second stage was not only inoperable
but empty as well.
                       -58-

-------
                 TABLE 6-3.  SECOND STAGE OUTAGE
                              December 16, 1974

Condition ACFM*
Second Stage
AP PH
S02 Outlet
Concentra-
tion (ppm)
% so2
Removal
Efficiency
Steady-State
Period Before
Outage (0500-
1200,12/16)      146,000      6.2    7.2      168          82.2
Second Stage
Outage (1300-
1400,12/16)       74,800       0     8        683          23.1
* At the inlet to the first scrubber stage.

     6.1.4  MgO Slaking and Recycle
          The MgO slaking equipment used in preparing the MgO
          slurry operated relatively trouble free.  The MgO belt
          experienced problems with slippage, but these were re-
          medied by adjustments.  The steam line to the MgO tank
          clogged once and the controller had one malfunction, but
          repairs were made without a shutdown.  On August 11, 1975,
          a crack developed in the steam control valve.  During the
          period when the steam line was not in use, a higher than
          normal amount of unreacted MgO was found in the second
          stage bleed.  When the steam line was put back into use,
          the amount of unreacted MgO returned to normal.  Further
          discussion of MgO slaking is covered in Section 6.2.2
          where its effect on system optimization is illustrated.
          The two rubber lined pumps (one operating and one stand-
          by) used for MgO slurry transfer and recycle of the second
          stage slurry normally operated reliably.  However, with
          one pump on the line it was not possible to maintain full
          design gas flow through the unit.  In order to provide
          sufficient slurry at design gas flows and SO^ loadings it
          was necessary to operate both pumps together.
                                 -59-

-------
     Leaks  in the  pumps  were  generally  remedied by repacking
     or adjusting  the  seals.   The main  problem experienced by
     the pump inlet  and  outlet lines was clogging because of
     an accumulation of  MgO.   This may  be  remedied by being
     able to isolate the individual pumps  and lines when they
     are not in service.   They could then  be cleared through
     a series of wash-out valves.  The  cleaning of these pumps
     and lines could be  part  of a routine  maintenance schedule.
6.1.5  Solids Removal Section for the Second Stage
     Centrifuge cover leaks and clogging of the centrifuge chute
     were the major problems with this equipment throughout
     the test program.  The leaks in the cover were probably
     caused by the abrasive material in the centrifuge feed
     water which wore away the carbon steel.  The centrifuge
     chute required almost continual attention at times,  de-
     pending on  the consistency of the centrifuge cake.   On
     days when the cake was wet or sticky,  the chute would re-
     quire periodic cleaning during each shift in order to
     prevent clogging.  The angle of the chute was changed once
     during the program and the vibrators were adjusted for
     continual operation but these changes  had little effect
     on the clogging problem.  As the test  program progressed,
     The operators started to wash the chute on a regular basis
     during their shift to prevent this problem.  Using a dif-
     ferent configuration or type of equipment may eliminate
     these problems in future designs.

     Approximately 1.5 percent of the total recycle of the se-
     cond stage was taken from the discharge of the recycle
     pumps to the centrifuge.  The centrifuge normally re-
     moved 50 percent of the solids in this liquid stream.
     During the course of the scrubber study, the flow to the
     centrifuge had to be diverted numerous times due to clog-
     ging of the centrifuge chute at higher gas flow and SO?
     loading conditions.  To initiate the assessment of the
     effects of these diversions, data taken during the centri-
                            -60-

-------
fuge repair on 11/15 were plotted in Figure 6-1 when the
centrifuge was out of service for about 2 hours and 40
minutes.  The centrifuge shutdown occurred at 0940.  To
prevent build-up of excess solids, the scrubber operators
reduced the gas flow to the unit at 1000.  It was further
reduced at 1030 when no progress was made on the repair.
The accompanying data sheet (Table 6-4) displays the
second stage Ap and inlet gas flow experienced during
this outage.  As a result of the operator action, SC>2 out-
let levels jumped from 120 ppm at 0900 to 250 ppm by 1000,
for a rise of over 100 percent.  They eventually peaked
at 340 ppm, but because of continued reduced gas flow,
they did not stabilize until 1500.  The lower pre-repair
levels of SC>2 outlet emissions were reached several hours
later.

Reduced gas flows were continued beyond the return of
the centrifuge to operation so that a reduction in the
solids that had accumulated might be affected.  Excessive
solids build-up on the system placed an undue strain on
the pumps and exposed pipes to erosion.  When a problem
with the centrifuge necessitated diversion, operators
attempted to circumvent the situation by first reducing
the flow of gas to the unit before and during the outage
to prevent solids build-up, and then by continuing this
reduced gas flow afterwards to work down the accumulated
solids.  Along with the reduction in flow, the operators
decreased the MgO slurry feed.

The centrifuge outage caused a reduction in S02 removal
efficiency because of the need to reduce the gas flow as
part of the remedial action.  Thus the two hour and 40
minute outage also caused a substantial build-up of
solids in the system, especially in the mother liquor,
which normally received centrate directly from the cen-
trifuge.  This is illustrated in Table 6-5.
                      -61-

-------
I
0\
ro
          100
                                                                           NOFM&L GEERKPION
           50
             07     08     09     10
11     12
13
14
15     16
17     18     19     20
                                                      •ELMS OF DRY

                                  REM3V&L EFFIdQ^CT DUREN3 CBUKEFUGE CX715VGE (11/15/74)

                                                      FIGUFE 6-1

-------
TABLE 6-4.  BOILER/SCRUBBER DATA  (NOV.  15,  1974)

Time Boiler Load
(MW)
0700
0800 169
0900
0930


; Outage
us
Cn
S
•H
•P
c
0)
u




'0945
1000 180
1015
1030
1045
1100
1115
1130
1145
1200 178
1215
1230
1245
^1300
1400 178
1500
1600 173
1700
1800 174
1900
2000 178
Scrubber A p Slurry
(2nd Stage) pH
7.4
8.0 7.4
7.4


5.8 6.4
7.3

3.0 7.1



7.3
3.0 7.0
7.1
5.2 7.1
7.0
5.2 7.0
7.2
7.0 6.9
S02 (ppm)
inlet/outlet
900/125
900/125
780/176
-
780/100
1150/250
1150/250
1450/340
1300/340
1300/340
1200/270
1100/275
1100/265
-
1050/210
1050/240
1050/270
900/190
900/190
900/180
900/170
800/160
800/160
SOj Removal
Efficiency (%)
86.1
86.1
77.1
-
87.2
78.3
78.3
76.6
73.8
73.8
77.5
75.0
75.9
-
80.0
77.1
74.3
78.9
78.9
80.0
81.1
80.0
80.0
                   -63-

-------
         TABLE 6-5.  PERCENT SOLIDS
Time
0800
1200
1600
Second Stage Bleed (%)
6.9
8.25
3.96
Mother Liquor (%)
1.16
3.99
1.13
The increase in solids measured in the mother liquor from
0800, which was before the centrifuge diversion, to 1200,
was 240 percent.  By 1600 hours that afternoon,  or by 3%
hours after the centrifuge was back on line,  the solids
had been decreased to its previous level.  In the case of
the second stage bleed, the increase at 1200 was not quite
as dramatic, but the solids were reduced by 50 percent by
1600.

Analysis of these results is somewhat hampered by the time
lag between test measurements.  If it had been possible
to follow more closely the rapidity of solids build-up
during the centrifuge outage, it might have been feasible
to extrapolate relationships between duration of outage,
extent of solids build-up, and minimum time necessary to
work down accumulated solids.  The four hour readings did
not provide any continuous assessment.

The final result of the two hours and 40 minute centri-
fuge repair on 11/15, then, was a five and one-half hour
period of higher than steady-state emissions.  Although
stability was attained at the end of the repair outage,
the emission level took several more hours to return to
thr prior steady-state concentration.  This effect is
shown in Table 6-6.
                      -64-

-------
              TABLE 6-6.  CENTRIFUGE REPAIR
                             Average Parameters
Condition
Second Stage
Ap pH
S02 Outlet
Concentration
(ppm)
% so2
Removal
Efficiency
Steady-State
Condition Before
the centrifuge
repair (0400-
0900, 11/15)    8.0     7.5          125              85.6
Centrifuge
Repair (1000-
1500, 11/15)    4.1     7.0          275              75.9
Because of the centrifuge repair, S02 removal efficiency
fell almost 10 percent, to 75.9 percent.  Correspondingly,
S02 outlet concentrations increased by 120 percent.  The
large drop in second stage Ap contributed substantially
to the efficiency decrease.  It should be noted, however,
that second stage pH dropped from 7.5 to 7.0.  This was
due to a cutback in MgO slurry feed in order to curtail
the accumulation of additional solids.

It is apparent that its capacity as a solid extractor
makes the centrifuge important for effective scrubber
operation.  The exact time period the scrubber can operate
without the centrifuge was not discernible from the data
of 11/15/74.

Other malfunctions that occurred in the solids handling
equipment were due primarily to centrifuge cake con-
sistencies which interfered with the dryer, the screw
conveyor and the bucket elevator operation.  The dryer
would clog when fed exceptionally wet cake; however,
this problem would normally clear up if the centrifuge
flow was diverted for a short time.  On one occasion
the scrubber was shut down because the dryer became so
clogged it had to be cleared manually.

                     -65-

-------
     The bucket elevator operations were not always reliable
     during the project.  An extremely wet or dry dryer pro-
     duct would cause the elevator to become ineffective.
     A wet product would overload the elevator and a very  dry
     product would be dusty and difficult to handle.  Buckets
     were changed once during the program, but became dis-
     torted and bent after a short time.

     One final malfunction that occurred in the solids handling
     equipment concerned the dryer ID fan belts which burned
     out on November 12, 1974.  When the belts were replaced,
     the fan would not start because of the water accumulated
     in the fan housing.  After this incident the draining of
     this housing was performed regularly as a maintenance
     function.  The water condensed and accumulated in this area
     whenever the dryer off gas temperature was below 212°F.

6.1.6  Process Control
     The process control of the scrubber system was relatively
     simple and thus created little problem in keeping the
     system functioning.  The liquid flow rates through the
     scrubber were constant and independent of gas load.  The
     MgO additive feed rate was varied to maintain the slurry
     pH at a preset point, about 7.  The main problem in the
     control room was with the pH meter which measured the pH
     at the discharge of the second stage re-circulation pump.
     During the test program the pot for the meter developed
     leaks and had to be patched.  In addition, the meter  be-
     came plugged at times with crystals and had to be manually
     cleaned.

     Other control equipment that required maintenance included
     the S02 analyzer probe which was replaced because it  was
     badly eroded.  Some of the flow rotometers froze and
     burst.  These were replaced or bypassed with spool pieces,
     when replacements were not available.  The MgO weigh  feeder
     was also found to be inaccurate and had to be recalibrated.
                           -66-

-------
     Control dampers were installed as indicated in Figure 3-2
     (Section 3 - Process Description) to regulate the amount
     of gas going through the scrubber.  Throughout the test
     period of October,  1974 to September, 1975, the dampers
     were frozen in position.  This left the ID fan after the
     scrubber as the only control device for varying the gas
     flow rate through the scrubber system.

6.2  Optimization
     In order to properly optimize the individual components
     within the process, the system should have been capable
     of operating at steady-state conditions for extended
     periods of time.  As can be seen from the previous section
     on operability, steady-state conditions were not attain-
     able for very long periods during the study.  The system
     was operated for a maximum duration of 120 hours before
     a shutdown was required due to equipment malfunctions.
     However, several attempts were made throughout the study
     to try and optimize various components within the system.

     Discussion of the optimization efforts of the FGD process
     centers on the second stage of the system.  Except for
     problems with materials of construction, the first stage
     of the scrubber performed very well during the testing
     program.  As a result no efforts were made to optimize
     the components of the first stage.

6.2.1  Second Stage Absorber
     To provide a better assessment of the influence of certain
     operating parameters, experiments were conducted at
     Dickerson modifying selected parameters and recording the
     results.  The first operating parameter to be changed was
     the re-circulated liquid flow rate to the tangential
     sprays and cones of the second stage.  These experiments
     were conducted on the 14th and 17th of December, 1974.
     Data collected for the variation of liquid flow rate
     appear  in Tables 6-7 and 6-8.

                          -67-

-------
                                   TABLE 6-7.  BOILER/SCRUBBER DATA
I
CTi
00
I

Date: 14 December 74 Time Span: 1400-1500 Test Condition:
Boiler ScrubberA Flue Gas Inlet
Load
Time (MW)
1400 146
1415
1430
1500
2nd Stage Flow* Scrubber S02
(in.H20) (ACFM) L/G pH (ppm)
6.2 159,700 31.9 6.0 1150
6.4 159,700 31.9 6.9 1140
6.4 159,700 31.9 6.9 1140
6.0 159,700 36.9 7.0 1190
Variance of Liquid Flow Rate
Outlet SO^ Removal 2nd Staqe
SO2 Efficiency
(ppm) %
205 82.2
200 82.5
200 82.5
195 83.6
Liquid Fli
(gpm)
5100
5100
5100
5900

* At the inlet to the  first  scrubber stage.

-------
                                    TABLE 6-8.  BOILER/SCRUBBER DATA
I
CTi

Date:
Time
0900
0950
1000
1035
1100
1130
1150
1200
1225
1245
1300
1320
1400
17 December 74 Time Span: 0900-1400
Boiler
Load
(MW)
151
162
174
182
182
182
ScrubberA
2nd Stage
(in. H?O)
3.7
8.2
8.2
8.0
8.7
7.4
6.2
6.0
6.6
8.3
8.5
9.5
9.7
Flue Gas
Flow
(ACFM) *
130,600
159,700
159,700
140,800
159,700
165,900
165,900
180,200
180,200
197,600
196,600
173,100
180,200
L/G
42.0
36.9
36.3
52.5
42.6
31.3
24.1
22.8
27.7
25.3
25.3
33.5
32.2
Test Condition:
Scrubber
PH
7.2
7.1
7.1
7.0
7.0
7.0
7.0
7.1
7.2
7.3
7.1
7.2
Inlet
SO2
(ppm)
790
1050
1050
1020
950
900
850
960
880
810
810
805
790
Experiments changing the liquii
flow rate in the scrubber 2nd
stage.
Outlet
S02
(ppm)
165
170
170
135
135
170
195
180
180
120
135
110
110
SO Removal
Efficiency
%
79.1
83.8
83.8
86.8
85.8
81.1
77.1
81.3
79.5
85.2
83.3
86.3
86.1
Liquid Flow
Rate
(gpm)
5500
5900
5800
7400
6800
5200
4000
4100
5000
5000
5000
5800
5800

      * At the inlet to the first scrubber stage.

-------
The experiment conducted on December 14 was run under
normal scrubber operating conditions.  As can be noted in
Table 6-7, a liquid to gas ratio (L/G)  of 31.9 was main-
tained until the last point where it increased to 36.9.
The Chemico scrubber design specified an L/G ratio in
units of gallons/(1000 ft3) at 117°F as 20 for the
first stage and 40 for the second.   It is apparent that
the second stage venturi was operated below the design
specifications during this experiment.   However, as the
L/G ratio approached 40, an increase in the scrubber
efficiency was observed.

In order to further evaluate the effect of the L/G ratio
and determine optimum value, further studies were conduc-
ted on December 17, 1974.  The difficulty in interpreting
these results lies in the fact that the Ap across the
scrubber second stage was not generally held constant.

In order to better depict the flows and efficiencies of
the 17th, Figure 6-2 is presented.   Figure 6-2 shows how
the S02 removal efficiencies followed the re-circulating
flow variations produced during the experiment.  As the
liquid flow rate increased so did the SO2 removal efficiency

By isolating the four readings in Table 6-7 from 1035 to
1150  the interaction of re-circulating flow and S02 re-
moval efficiency at constant pH can be studied.  As is
shown during this period in Table 6-9,  the pH of the ab-
sorber remained constant at 7.0.  The re-circulation rate,
however, was steadily decreased from the 7000 gpm level
at 1035 to the 4000 gpm mark at 1150,  the result was a
drop in efficiency of almost 10 percent.  The second  A P
also dropped reflecting the fall in the re-circulaion rate.
                      -70-

-------
            Missing
        Data Points
0900
1000
1100
1200
1300
1400
               LIQUID FLOW RATE VARIATIONS
                        12/17/74

                       FIGURE 6-2
                        -71-

-------
         TABLE 6-9.
LIQUID FLOW RATE CHANGES
   December 17, 1974


Time
1035
1100
1130
1150



7
7
7
7


pH
.0
.0
.0
.0

Gas

Flow
(ACFM)
140
159
165
165
,800
,700
,900
,900


Second
StageAp
8
8
7
6
.0
.7
.4
.2
Liquid
Flow
Rate
(gpm)
7400
6800
5200
4000


S02
Removal
Efficiency
L/G
52.
42.
31.
24.

5
6
3
1

86.
85.
81.
77.
%
8
8
1
1

The second operating parameter to be changed on the second
stage was the  pressure drop across the throat of the
venturi scrubber.  Since the throat of the scrubber is of
a fixed size and the liquid flow rate is normally at a
constant volume, the only other parameter which affects
the pressure drop across the throat is the volume of gas
flowing through the venturi.  With this in mind> tests
were conducted on January 27, 1975 to assess the affects
of varying gas flows at a constant re-circulating rate
of 5000 gpm.
Gas flow rates approximately equal to the design specifi-
cations were run through the scrubber for approximately
one hour, and were then maintained at lower levels for
five additional hours.  Higher SOj removal efficiencies
were obtained during the operation at high flows.  Data
shown on Table 6-10 indicate that with lower gas flows in
the 100,000 ACFM range, the SO2 removal efficiencies were
approximately 80 percent.  When the gas flow increased to
290,000 ACFM the efficiency rose to over 90 percent.

The close correlation that exists between flue gas flow
rate, second stage Ap, and the unit's efficiency through-
out this period of high gas flows is illustrated very well
in Figure 6-3.  At 0900, when the flue gas flow rate was
above 290,000 ACFM, second stage Ap was 13.0 inches H20

                      -72-

-------
w
                               09    ID    1.

                              HOUR OF DAY

                              HIGH GAS FLOW
                                 1/27/75

                               FIGURE 6-3
12
13
14
                                  -73-

-------
TABLE 6-10.  BOILER/SCRUBBER DATA  (1/27/75)

Time
0600
0700
0800
0900
0915
0930
0945
1000
1015
1030
1045
1100
1115
1130
Boiler Load
(MW)
116
163
176
162



116



138


Scrubber Ap
(2nd Stage)
0.7
1.8
0.2
13.0



10.8



10.2


Flue Gas
Flow Slurry
(ACFM) pH
169,400 7.4
188,300 7.4
141,200 7.5
291,800 7.5
291,800
291,800
291,800
242,200 7.4
255,000
255,000
255,000
242,200
242,200
222,400
SO2 (ppm)
inlet/outlet
1000/280
1000/280
900/240
900/63
-
900/63
900/50
910/80
900/75
-
900/90
940/105
900/110
—
SOo Removal
Efficiency (%)
72.0
72.0
73.3
93.0
-
93.0
94.4
91.2
91.7
-
90.0
88.8
87.8
—

-------
TABLE 6-10.  BOILER/SCRUBBER DATA  (1/27/75)(Continued)

Boiler Load Scrubber Ap
Time (MW) (2nd Stage)
1145
1200 174 8.0
1220
1235
, 1250
^_ t
^ 1305 175 7.8
1320
1345
1400 174 8.0
Flue Gas
Flow Slurry
(ACFM) pH
218,100
207,400 7.2
207,400
207,400
200,400
207,400 7.3
207,400
197,600
218,100 7.1

SO2 (ppm)
inlet/outlet
1000/120
1020/130
1000/120
-
1000/120
1020/125
1000/130
-
1020/125

SC>2 Removal
Efficiency (%)
88.0
87.3
88.0
-
88.0
87.7
87.0
-
87.7

-------
and the unit efficiency was a very high 93 percent.  How-
ever, once the gas flow was decreased to 242,200 ACFM at
1100, second stage Ap fell to 10.2 inches H-O and the
efficiency dropped to 88 percent.

It would have been valuable if the rapidity of solids
build-up in the absorber could have been monitored when
the gas flow was high.  It would have provided some measure
of the requirements to be placed on the centrifuge, and
possibly delineated a constraining factor on continued high
gas flow operation.  From the data available it is known
that the solids iji the second stage bleed were 1.39 percent.
Solids levels rose to 7.51 percent at 1200, when the
efficiency was 88 percent.  Greater solids formation at
higher efficiencies was observed.  It can only be spec-
ulated as to what the solids build-up amounted to at 0930
when efficiency was 93 percent, but if above 10 percent,
it probably placed undue strain on the pumps and pipes.
This possibility would have to be investigated fully in
conjunction with the ability of the centrifuge to work
down the solids before making a final assessment on the
benefit of a high gas flow for this demonstration plant.

The data from the December 17th tests (Table 6-8) also
demonstrated that efficiency rises by increasing gas
flow and maintaining the liquid flow rate constant.  The
readings for 1225 and 1245, reproduced below, show the
same liquid flow rates of 5000 gpm, but differing gas
flows.  Since the gas flow at 1245 was higher than at
1225, second stage Ap increased, and S02 removal ef-
ficiencies rose by almost 6 percent in 20 minutes.
                      -76-

-------
	TABLE 6-11.  TEST RESULTS - DEC. 17, 1974

       Flue Gas       Second    Liquid Flow  SO, Removal
Time   Flow (ACFM)   StageAP   Rate (gpm)   Efficiency(%)
1225
1245
180,200
197,600
6.6
8.3
5000
5000
79.5
85.2
In concluding the experiment on liquid flow rate changes
(Table 6-8), high gas flows were combined with high
liquid flow rates, and higher efficiencies were the re-
sult.  At 0950, a 5900 gpm liquid flow rate and an 8.2
inch H20  A P produced an 83.8 efficiency, whereas at
1320 a 5800 gpm liquid flow rate and a 9.5 inch H2O A?
produced an 86.3 percent efficiency.  It was the higher
gas flow rate at 1320 that increased the second stage  A P
and produced the greater efficiency.

The third parameter that was changed on the absorber was
the restrictor in the throat of the second stage venturi.
During the boiler shutdown between February and August
1975, several modifications were made to the system, one
of which was the removal of the restrictor in the second
stage venturi throat.  This change was made by Chemico
in order to provide data on operation at a reduced pres-
sure drop while maintaining a design gas flow rate.

In order to demonstrate the effect of removing the throat
restriction, Table 6-12 provides data from a test run on
August 26, 1975.  It is seen that there is a dramatic de-
crease in the A P for a given flow rate with a correspond-
ind decrease in SC>2 removal efficiency.   The data in
Table 6-13 are extracted from Tables 6-8 and 6-12 to demon-
strate this point.
                      -77-

-------
                                   TABLE 6-12.  BOILER/SCRUBBER DATA
oo
I

Date: 26 August
Boiler
f — -a
xjucKa
Time (MW)
0400 176
0415
0500 183
0515
0600 180
0700 176
0710
0715
0716
0717
0718
0719
0720
0730
0800 177
0815
0900 ,176
1000 178
1030
1045
1100 180
1200 184
1230
75 Time Span: 0400-1400
Scrubber A p Flue Gas
Secund St
-------
TABLE 6-12.   BOILER/SCRUBBER DATA   (CONT.)

Date:
Time
1245
1300
1330
1345
1400
* At
i
10
: 26 August 75 Time Span: 0400-1400 Test Condition: Rapid Velocity Chanc
Boiler Scrubber A p Flue Gas Inlet Outlet
Load Second Stage Flow Scrubber SO2 SO2
(MW) (in.H20) (ACFM)* pH (ppm) (ppm)
173,000 7.1 1200 370
185 173,000 1200 350
198,700 1120 320
198,700 1100 300.
185 3.6 198,700 6.8 1100 . 300
the inlet to the first scrubber stage.


SOo Removal i
Efficiency
69.2
70.8
71.4
72.7
72.7




-------
                     TABLE 6-13.   ALTERATION OF Ap
Date
L2/17/75
8/26/75
Time
1035
1100
Ap
8.0
1.6
Gas (ACFM)
140,800
140,800
SO2 Removal Eff.
86.8
67.2
     Without additional details to describe the design of the
     venturi, further extrapolations as to the energy required
     Ln the form of a pressure drop across the venturi to pre-
     dict S02 removal efficiency cannot be made.

6.2.2  MgO Slaking
     No deliberate attempts were made to change any of the para-
     meters in the MgO slaking operation.  The control system
     was set up so that the pH of the second stage recycle line
     was maintained at approximately 7 throughout the test program.

     On August 11, 1975 the malfunction of the steam control
     valve on the MgO slurry tank provided the opportunity to
     observe the effect of reducing the amount of steam to the
     slaking process.  A result of this heat reduction was a de-
     crease of the efficient usage of MgO.  This is clearly illus-
     trated in Figure 6-4 which shows the percent of unreacted MgO
     appearing in the centrifuge cake during a period of normal
     heating, and during a period when the heating system was in-
     operable.

     The large amount of MgO in the centrifuge cake eventually
     created a major problem in the dryer.  On August 15, 1975,
     the dryer was plugged with a rock-hard material.

     Subsequent analysis of this material indicated the existence
     of a large concentration of inerts,  which were hypothesized
     to be oxysulfate.   An oxysulfate cement is formed by the re-
     action of magnesium oxide which has  been produced by the
     calcination of a magnesium compound, with a  solution of
     magnesium sulfate of suitable concentration  .   Since

                             -80-

-------
       16
g  8
w
     W
     O<
                   08        16
                     1/12/75
                                                   MgO SLURRY  TANK TEMPERATURE:  155 F
                                  00
08        16
  1/13/75

DATE & TIME
00
08        16
  1/14/75
i
00
                                                   MgO SLURRY TANK  TEMPERATURE:  114~F
        n
                             08        16
                               8/11/75
                                                       08         16
                                                          8/12/75
                  UNREACTED MgO IN CENTRIFUGE CAKE AS .A FUNCTION OF TEMPERATURE

                                           FIGURE 6-4
                                         08

-------
     a large amount of free water was present during this  run
     and available MgO was present,  the 10-20% concentration
     of MgSO. -71^0 in the free water reacted with the available
     MgO to form the oxysulfate cement.

     As a result of the problems incurred with the breakdown
     of the steam control valve and  the evaluation of the  re-
     sultant data collected, it becomes evident that the MgO
     slurry tank must be operated at some optimum temperature
     from an economical and operational standpoint.  The object
     in maintaining this temperature is to arrive at an optimum
     amount of MgO of sufficient activity in the re-circulation
     lines and especially in the centrifuge cake.  Since these
     observations were made at the end of the testing program,
     insufficient time was available to study this problem fur-
     ther.

602.3  Solids Removal System
     Throughout the operating period of the scrubber system,
     there was no control system to regulate the solids con-
     centration in the second stage  absorber.  Samples were
     collected, however, at 4-hour intervals to monitor the
     percent solids for purposes of analyzing the perfor-
     mance of the system.

     Upon reviewing the data collected prior to the comple-
     tion of the scrubber testing in January, 1975, Chemico
     stated that they wished to operate the centrifuge at  a
     different rotational speed to determine removal effici-
     ency at a second separational force.  Table 6-14 shows the
     data collected on December 6-8, 1974 from operations  at a
     higher torque, and from August 12-14, 1975 from operations
     at lower torque.  No definite statements can be made  con-
     cerning the solids removal efficiency at rates greater
     than 24 g's; however, as the separation force decreases
     from this point, the efficiency also definitely decreases.
                          -82-

-------
                               TABLE  6-14.   SOLIDS REMOVAL EFFICIENCY DATA
                                 Data for Dec. 6-8,'74 and Aug. 12-14,'75
00
OJ
               Higher Torque Operation
                                  Mother
               2nd Bleed          Liquor
               % Solids   Torque  % Solids
                           % E
                               Lower Torque Operation
                                                  Mother
                               2nd Bleed          Liquor
                               % Solids   Torque  % Solids
                                                    % E
12/6
MidN.




12/7





12/8





9.
7.
7.
8.
11.
13.
10.
10.
11.
9.
10.
14.
10.
11.
11.
11.
12.
11.
07
62
04
32
92
29
36
06
18
34
90
57
89
98
17
88
08
95
58
40
40
50
52
46
46
50
50
40
40
45
44
44
40
44
24
27
8.91
2.72
3.79
3.14
2.75
3.20
5.24
3.92
4.08
3.08
3.70
4.01
5.36
5.49
4.18
4.22
NA
3.68
1.
64.
46.
62.
76.
75.
49.
61.
63.
67.
66.
72.
50.
54.
62.
64.
—
69.
7
3
2
2
9
9
4
0
5
0
1
4
8
2
6
5

2
8/12 3
MidN . 4
3
4
3
6
8/13 7
7
8
7
7
9
8/14 8
19
2
2
3
4
.5
.0
.14
.20
.01
.81
.19
.76
.25
.23
.97
.28
.83
.79
.56
.61
.07
.77
22
26
24
28
32
45
52
43
42
32
36
32
8
OFF
3
1
2
14
2.92
0.39
0.39
NA
0.67
0.88
2.87
1.91
2.23
2.51
2.82
3.35
7.03
3.45
2.29
2.59
3.32
4.39
16.6
90.3
87.6
—
77.7
87.1
60.1
75.4
73.0
65.3
64.6
63.9
20.4
82.6
10.5
0.8
—
8.0
      Average
10.76
43
4.20
6.33
26
2.59

-------
     A second parameter that is of importance  in the  operation
     of the centrifuge is the amount of magnesium sulfite that
     is in the hexa-hydrate form as opposed to the trihydrate
     form.  The hexa-hydrate form has a large  crystalline
     structure which allows the centrifuge and dryer  to operate
     more efficiently.  Experimental studies were conducted by
     YRC to determine the percent combined H20 in the centrifuge
     cake that was of the hexa-hydrate as opposed to  the tri-
     hydrate form of magnesium sulfite.  The test results indi-
     cate that at least 80% of the product in  the centrifuge
     cake was of the form
     Observations that were made on a similar magnesium oxide
     scrubber at Boston Edison's Mystic Station indicated
     that the tri-hydrate form of magnesium sulfite was the
     predominant form of the product.  To further investigate
     this reaction,  the U.S. EPA commissioned Radian Corpora-
     tion to study the kinetics and equilibrium of the hydrate
     formations.  The report on this study will soon be pub-
     lished.

6.3  Performance
     The Dickerson MgO system was capable of removing 90% of
     the sulfur dioxide produced when burning coal containing
     2% sulfur.

6.3.L  SO2 Removal Efficiency
     From the beginning of full scale testing on October 15,
     1974 to the completion of testing on January 27, 1975
     the scrubber system was normally able to attain effi-
     ciencies of between 78-83%.  Maximum efficiencies of 96-
     97% were obtained at high flue gas flow rates on short
     duration runs of several hours, but difficulties in
     running the MgO feed system and solids separation sys-
     tem for the second stage at high flow rates necessi-
     tated that the system generally be run at 75% of the de-
     signed flue gas flow rate.
                           -84-

-------
     During the down period of January 27,  1975 to August 11,
     1975, the restrictor plate in the venturi throat was  re-
     moved to observe the performance at a  lower A p.  From
     August 11, 1975 to September 27, 1975, an average ef-
     ficiency of between 70-75% was attained.   No attempts
     were made to run the system at high gas flow rates due
     to the problems with the feed system and the solids sep-
     aration system for the second stage.

     The parameter  that affected the SO- removal efficiency
     the most was determined to be the pressure drop across
     the venturi throat.  This parameter is a measure of energy
     usage required to make the system work.  In order to reach
     efficiencies greater than 90%, a pressure drop of at least
     11 inches of H20 was required.  This value was achieved
     with close to design gas flow rates flowing through the
     venturi at an approximate L/G of 20.  A second parameter
     that was studied was the liquid to gas ratio.  It was
     found that doubling the volume of recirculating slurry at
     a pH of 7.0 increased the SO- removal  efficiency by only
     10 percent at lower gas flow rates; however, an increase
     of 10 to 20% in the SO2 removal was incurred by increasing
     the pressure drop across the venturi throat with higher
     gas flow rates.

6.3.2  Particle Removal Efficiency
     The provision to by-pass the ESP and send flue gas with
     a heavy concentration of particles to  the scrubber worked
     very well in demonstrating the ability of the FGD system
     to attain a high particle removal efficiency in excess of
     99%.  One concern that is coupled with this high removal
     efficiency is the possible build-up of inert flyash in
     the second stage solids.  Since the FGD system was not
     operated enough to attain a high recycle rate of MgO,
     no data were recorded that indicated that there was a
     flyash build-up problem.  As with all  power plant scrubber
                           -85-

-------
     particle removal systems,  the problem of the ultimate
     disposal of the flyash slurry from the first stage must
     be given careful consideration due to its low pH and high
     chloride concentration.

6.3,3  Duration of Scrubber Performance
     Throughout the full scale testing program time period
     of October 18, 1974 to January 27, 1975 and August 11,
     1975 to September 27,  1975, the scrubber was operating
     approximately 53% of the time.  Many of the scrubber
     outages were the result of leaks which developed in the
     first and second stage recycle systems, and also due to
     the lack of MgO raw material make-up.  In order for a
     system of this size to operate without interruption, at
     least twice as much material storage must be available
     to counteract the shipment problems which occurred
     throughout the project.  On-site storage was only 100
     tons which at design conditions was about a month's
     supply.  A second storage problem arose with the dis-
     posal of the magnesium sulfite product.  A 200 ton stor-
     age silo was employed at the Dickerson site which proved
     to be inadequate due to the erratic operation of the MgO
     regeneration station in Rumford, Rhode Island, which would
     certainly not be representative of a commercial unit.
     As a result of experiencing these storage problems, it  is
     apparent that a reliable regeneration facility is neces-
     sary to make the MgO FGD process a viable system.
                           -86-

-------
7.0  CONCLUSIONS

The test program has shown that the S02 removal efficiency of the
MgO venturi scrubber is principally dependent upon both the pressure
drop, and the liquid to gas ratio of the second stage venturi ab-
sorber.  Removal efficiencies of over 90 percent were attained with
an 11 inch (H-O) pressure drop.

The particle removal efficiency of the first stage was greater than
99 percent when the flue gas was taken directly to the scrubber from
the boiler, and not pre-conditioned by the ESP.

The overall performance of the scrubbing system was satisfactory,
aside from difficulties experienced with materials and equipment
(which have been documented herein).  During transient operation,
operational problems and high emission levels were generally
normalized soon after the upset occurred.  Sustained operation
was never experienced, and as a result data obtained are only
representative of those short periods studied.

Availability percentages were rather low but this was only partially
due to the basic scrubber design.  The distance and nature of the
MgO recovery operation often caused scrubber shut-downs due to lack
of raw materials.  Low availability was also due to:

     •  Lack of proper recirculation systems.
     •  Lack of pipe linings.
     •  Auxiliary equipment problems.
     •  Lack of sufficient number of operators.
     •  Boiler shut-downs.
                                -87-

-------
If these deficiencies were corrected, efficiency and availability
would have been significantly improved.

The aforementioned problems also reduced the time and effort that
should have been spent on experimentation and optimization of the
process.  For the most part, work done to test the operation proved
successful.  An example of this would be the study of liquid to gas
ratios, and high gas flows.  Unfortunately, there were not enough
such investigations to fully characterize and optimize the process.

It is recommended that consideration be given to further testing of
the MgO process in order to better characterize the system under
longer term operation and to demonstrate commercial availability.
                                -88-

-------
                           REFERENCES
1.  YRC Report 4-8864:  Preliminary Report for the Evaluation
    of Particulate Emission Control at PEPCO's Dickerson
    Station.  PEPCO Report dated 10/31/75.

2.  Federal Register, Vol. 37, No. 247, Dec. 23, 1971.
                                 -89-

-------
         Conversion Factors:  British to SI Units
             To Convert
       From
   To
Length
Mass
Voluire
       inch  (in.)
       foot  (ft.)
       pound (Ib.)
       ton
       grain
       cubic foot
       (CF, ft3)
       gallon  (gal)
meter  (m)
meter  (m)
kilogram  (kg)
kilogram  (kg)
kilogram  (kg)
cubic meter(m )

cubic meter(m )
Energy
       British thermal
       unit  (Btu)     calorie  (cal)
Temperature
       Fahrenheit(°F) Celsius  (°C)
       Celsius ( C)   Kelvin  (K)
multiply by 0.0254
multiply by 0.3048
multiply by 0.4535924
multiply by 907.1847
mulitply by 0.0000648
multiply by 0.02832

multiply by 0.003785



multiply by 251.9958
                °C = 5/9  (°F - 32)
                 K = °C + 273.16
                             -90-

-------
        APPENDIX A

 SCRUBBER EQUIPMENT LIST
           AND
EQUIPMENT SPECIFICATIONS
             -Al-

-------
Scrubber Equipment List

Item Description

MgO Make-Up Tank
Dust Collector-MgO Silo
Thickener
Transfer Tank
Distribution Box
Sump Tank
Mother Liquor Tank
Dust Collector-Dryer
MgO Storage Silo
MgSOs Silo
MgO Feed Pump
First Stage Recycle Pump
Second Stage Recycle Pump
Underflow Pump
Transfer Pump
Sump Pump
Mother Liquor Pump
Induced Draft Fan
MgO Agitator
Mother Liquor Agitator
MgO Weigh Feeder
Dryer Feed Conveyor
Dryer Discharge Conveyor
Dryer Discharge Elevator
MgS03 Weigh Feeder
Two-Stage Venturi Scrubber
Mist Eliminator
Variable Speed Coupling
Centrifuge
Rotary Dryer
Dryer I.D. Fan
Instrument Air Dryer
Code No.

G-101
G-102
G-201 A,B
G-202
G-203
G-204
G-301
G-401
1-101
1-401
J-101 A,B
J-201 A,B
J-202 A,B,C
J-203 A,B,C,D
J-204 A,B
J-205
J-301 A,B
K-201
M-101
M-301
0-101
0-401
0-402
0-403
0-405
R-201
R-202
R-203
R-301
R-401
K-402
V-101
Quantity

   1
   1
   2
   1
   1
   1
   1
   1
   1
   1
   2
   2
   3
   4
   2
   1
   2
   1
   1
   1
   1
   1
   1
   1
   1
   1
   1
   1
   1
   1
   1
   1
Motor Horse-
power (HP)
   10
   350
   250

   125
   30
   20
   3500
   5
   3

   1
   2
   2
   200
   40
   100
                             -A2-

-------
GENERAL SPECIFICATIONS - SG>2 REMOVAL SYSTEM

EQUIPMENT

1.  MgO System

MgO Make-Up Tank  (G-101)
MgO Storage Silo  (1-101)
MgO Feed Pumps and Motors  (J-101 A & B)

Agitator (M-101)

One paddle type agitator (Denver, or equal), including enclosed
reducer with coupling, shaft, three 8" deep horizontal paddle
arms 7' diameter and 45 degree angular paddle in tank conical
section, beam type superstructure V-belt drive, drive guard
5 HP, 900 rpm-TEFC motor and motor base.  Includes seal and
seal plate to mount on tank cover around the shaft.  Paddle
speed 8 rpm, reducer ratio 48 to 1; wetted parts mild steel
construction.

MgO Weighing System (0-101)

One gravimetric feeder which provides a continuous measurement
of weight through a scale; compares the measurement signal with
the set point through suitable control instrumentation, and
actuates a hopper gate to provide a constant feed of material.  A
section of the constant speed weight belt is weighed by means of
mechanical levers and a scale beam.  Beam deflection is trans-
mitted mechanically via a link connection to a regulator that
adjusts the feed gate.  Unit includes self contained belt feeder
mechanical weight control loop, totalizer, totally enclosed pulley
transmissions, and static test weights, capacity 0.5 to 1.5
Standard Tons Per Hour  (STPH).

MgO Supply Conveyor (0-102)

One conveyor handling 25 STPH of magnesium oxide with bulk density
of 25 Ibs/cu.ft. from the truck unloading hopper to the silo
feed elevator.

2.  Absorption System

1st Stage Recycle Pumps and Motors (J-201 A,B)
2nd Stage Recycle Pumps and Motors (J-202 A,B,C)
I.D. Fan and Motor (K-201)
Scrubber (R-201)

3.  Centrifuge System

Mother Liquor Tank (G-301)
Mother Liquor Pumps and Motors (J-301 A,B)

Centrifuge (R-301)

One 36" x 72" carbon steel solid bowl continuous centrifuge,
(Bird or equal), including 200 HP, 460 volt, 3 phase, 60 cycle

                             -A3-

-------
TEFC motor with high thermal capacity.  A main bearing forced
oil circulating system is provided with pump, drive motor, oil
filter, heat exchanger, pressure switch and gauge, and oil
reservoir.  An outlet chute is included.
4.  Dryer System

MgS03 Silo (1-401)
Rotary Dryer (R-401)
Size of dryer
Shell plate
Feed end head
Number of riding rings
Riding rings
Support rollers
Thrust, roller
Hammers
Feed end chamber
Dryer Dust Collector (G-401)
Description
One rotary dryer, to produce
the anhydrous products MgSOs,
MgSC>4 and MgO as follows:
8'0" diameter x 50'0" long
V
5' - 0" diameter x V plate
2
8'10" diameter x 7" face
20" diameter x 9" face
16" diameter x 2V face
2 sets of 8
Breaching where the feed con-
veyor enters the dryer
One cyclone with scroll outlet for 97% removal, plus rotary
discharge valves.  The fines collected by the collector will re-
turn directly to the dryer product conveyor.

Dryer I.p. Fan (K-401)

One induced draft fan, with inlet and outlet flanges, inspec-
tion door, drain, dampler, V-belt drive, drive guard, and 100 HP,
3 phase, 60 cycle, 230/460 volt, 1,800 rpm, TEFC, motor.
Fan Performance Data

Volume
Static Pressure
Speed

Dryer Combustion Chamber
26,500 CFM @ 400 F
8" S.P.
1,800 rpm
One direct fired air heater approximately 6' - 0" O.D. x 18 '-0"
long, etnd designed to operate with the following:
Maximum Heat Release
Inlet Temperature
Combustion Chamber Temp.
Site Elevation
Operating Furnace Pressure
Fuel
Maximum Oil Viscosity
Type Fuel Oil Atomization
Burner Turndown
Insurance Requirements
26.3 10° Btu/hr
70°F
1,600 F
Sea Level
Balanced
No. 2 fuel oil
40 SSU, constant
Air
5:1
F.I.A.
                             -A4-

-------
Fuel Oil Supply for Combustion Equipment (R-401)

A duplex fuel oil pumping and straining set, designed to meet
the following conditions will be provided to supply fuel oil to
the air heater burner:

Fuel Oil                         No. 2
Design Capacity                  3 gpm
Pump Discharge Pressure          125 psig
Maximum Suction                  Plus 30 psig
                                 Minus 13" Hg
Electric Service                 440 volt, 3 phase, 60 cycle

Dryer Feed Conveyor (0-401)

One 12" diameter x 5'0" long heavy duty ribbon feeder conveyor,
complete with 3 HP drive.

Dryer Discharge Elevator (0-403)

One elevator which elevates 5 STPH of dried magnesium sulfite
with a density of 50 Ibs/cu.ft. discharging from the dryer to
the magnesium sulfite bin.

SCRUBBER INSTRUMENTATION AND CONTROLS

The system has two separate control panels as follows:

1.  The scrubber/absorber control panel (SCP) located in the
    prefab building south of the mist eliminator vessel.

2.  Main control panels (VB and BB) located in the main control
    room of the existing powerhouse building.

Scrubber/Absorber System Control Panel

The following controls are located on the control panels located
in the prefab building and their names and functions are des-
cribed.

PDR-1       pressure drop recorder for first stage of scrubber
            absorber
FRI, 1,2    first stage recycle liquor flow rate indicator
LIC 1       level indicator - controller for first stage scrubber
LIC 11      level indicator - controller for transfer tank
HIC 10      manual loader for bleed from first stage to dis-
            tribution box
WI 28,29    torque indicators on thickener rakes A and B
PDR 3       pressure drop recorder for second stage of scrubber/
            absorber vessel
FIC 5       flow indicator - controller, MgO slurry to scrubber
HIC 4       manual loader for bleed from second stage to centri-
            fuge
LIC 2       level indicator - controller scrubber 2nd stage
WR 11       torque recorder, centrifuge
LIC 7       level indicator - controller,MgO make up tank
LIC 8       level indicator - controller,  mother liquor tank
FR 20       flow recorder,  mother liquor to MgO tank
                             -A5-

-------
TR 8
TIC 8
PIC 12
FR 23
TJR 4
WCIQ 18
TISH 1A,1B

FI 7

PDI 2
PDI 4
FI 6
FI 4

FI 3

AIC 1
AR 2
AI 2
WCIQ 17
TISH 9

II 9A,IJ
ZI - 1A
HS 9
II 10A,B,C
HS 14
HS 15
HS 5
temperature recorder, dryer outlet gas
temperature indicator - controller, dryer outlet gas
pressure indicator - controller, dryer outlet gas
flow recorder, fuel oil flow to dryer
six point temperature recorder:

1.  flue gas, dryer exit
2.  product discharge, dryer
3.  cyclone inlet, dryer
4.  spare
5.  spare
6.  spare

controller, totalizer MgSO-j feeder
temperature indicating switches, 2nd stage scrubber
inlet
flow indicator, make up liquid to 1st stage from
transfer pumps
mist eliminator pressure drop, 1st stage
mist eliminator pressure drop, 2nd stage
flow indicator, centrifuge feed
flow indicator 2nd stage scrubber, upper cone,
recycle loop
flow indicator 2nd stage scrubber, lower cone,
recycle loop
SC>2 inlet/outlet concentration indicator
pH recorder, bleed to centrifuge
pH indicator, bleed to centrifuge
controller totalizer, MgO weigh feeder
temperature indicating switch, dryer combustion
chamber outlet
ammeters, 1st stage scrubber recycle pumps
scrubber cone position indicator
transfer pump selector switch
ammeters, 2nd stage scrubber recycle pumps
mother liquor pumps, selector switch
MgO makeup pumps, selector switch
hand selector switch, recycle pumps, 1st stage
Main Control Panel

The following controls are located in the control room in the
main building.  Their names and functions are given belowt

PDA 1       plumb bob position and pressure differential,
            1st stage
PAL 20      low pressure alarm ID fan fluid drive
TAH 5       high temperature alarm ID fan drive bearings
TAH 10      high temperature alarm ID fan fluid drive
            accessories
XAH 7       alarm, ID fan vibration
IA 8        ID fan motor trip
FALL 2B     low low flow, scrubber recycle, first stage
FALL 7B     low low flow scrubber makeup, first stage
TAHH 2B     high high temperature, gas inlet 2nd stage
ZI IB       position indicator, plumb bob
                             -A6-

-------
HS 12       auto manual station, plumb bob
HS 4        precipitator mode selector switch
HS 17       raise lower switch, plumb bob
TISH 5      alarm annunciator motor, fan and fluid drive bearings
II 7        ammeter, ID fan motor
HS 22       start, stop switch ID fan
PDIC 1      pressure indicator controller, plumb bob, 1st stage
HS 6        hand selector switch, recycle pumps, 2nd stage
HS 16       selector switch, pond water return pump
                             -A7-

-------
-A8-

-------
  APPENDIX B
DATA TABULATION
   -Bl-

-------
DATA TABULATION

These tables represent the hourly data obtained during the
testing period.  When data are missing, an (NF) or an asterisk
(*) appears.  An NF indicates that the instrument used to measure
the parameter was not functioning.  The asterisk indicates that
the datum was not obtained, usually for a reason explained in
the footnote, or otherwise unknown.
                             -B2-

-------
                                                                   HOURLY DATA
 I
W
U)
Inlet
Date Time
1974
11-1 Scrubber
11-2 SiTubbiT
11-3 Scrubber
11 -'I Scrubber
11-5 Scrubber
11-0 Scrubber
U-7 Scrubber
11-8 Scrubber
11-9 Scrubber
11-10 Ol'lS
0220
01(10
03U5
0'1'IS
OS'IS
OO'IS
07 'IS
08 'IS
09 US
10'IS
11US
12US
13US-19US
20US
21U5
22U5
23'IS
11-11 OOUS
01U5
0220
Scrubber
ACFM x 2nd
MW JJ100 ^ P
Down,
Down
Down
Down
Down
Down
Down
Down
Down
178
J78
158
IU8
151
151
ISO
151
101
173
17 U
172
170
100
173
17 'I
108
105
1'|7
1'I7
138


NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
*
NF
NF
NF
NF
NF
NF
NF


U.O
'1.8
O.S
0.5
5.5
5.5
'1.9
0.2
0.0
0.2
1.0
1.0
3.5
*
2.0
'1.2
'1.2
5.0
5.0
1.0
0.0
Stage


Nr1
Nr
Nr
0. 3
o.u
o.o
7.3
7.0
7.0
o.s
0.8
0.8
7.1
*
0.9
7.0
0.8
7.0
O.S
0.0
5.0
S02
ppm


Nr
Nr
NC
000
080
7 '10
700
700
1050
Nr^
900
920
970
Nl'3
1050
lO'lO
1020
1000
1000
1000
1200
INI
NOX
ppm


Nr
Nr
Nr
uoo
'100
380
390
390
UOO
MI-
NT
NT
NT
NF
390
too
390
380
380
370
220
,cr
C<>2


. Nr
Nr
NT
11.75
13.5
15.5
15.0
1 S.O
.10.0
NT
.15.3
1'I.S
13.0
Nr
1'l.S
Ib.S
10.5
It. 5
15.0
I'l.O
Nr1'
OUTLET % SOp
02
%


Nr
NT
NF
7.0
0.8
0.0
7.0
0.0
0.8
NT
7.8
7.7
7.3
NT
9.5
9.5
9.0
10.0
9.0
9.2
NT
S02
ppm


NT
150
125
ISO
100
100
150
I'll)
195
NT
I'lO
185
210
NI'
220
220
220
225
220
220
1000
NOX
ppm


NT
300
.350
UOO
UOO
380
UOO
380
UOO
NT
Nr
Nr
Nr
NF
330
300
350
3 tO
3 to
NF
NF
C02


NF
12.2
13.0
12.5
13.5
10.0
15.0
1'I.S
10.5
Nr
10.5
11.0
11.5
Nr
13.0
15.0
15.5
13.9
I'l.O
NF
NF
02
%


Nr
8.5
8.7
7.0
0.8
7.0
7.0
0.8
0.8
NT
>10.0
HO.O
9.5
NF
>10.0
10. 0
9.8
9.8
9.8
NF
NF
Removal
Efficiency


-
-
-
77.3
70.5
78. U
78.0
80.0
Bl.U
-
8U.U
79.9
78. U
-
79.0
78.8
78. U
77.5
78.0
78.0
-
                          •I pll olpctrodp broken; Start up
                          2 Watnr In sample lines
                          3 Wator tn analyzer lines
                          '' Smibbpr down 0220; Watpr leaks

-------
                                                  HOURLY DATA
Date

11-12
11-13
11-14
Aiu.tii_ GUJE uuDcr •*• *'"*-* •*-'•*-
ArFM x 2nd Stage SO2
Time
MM
Scrubbrr
2010
2030
2130
2230
2330
0030
0130
0230
0330
0430
0530
0630
0730
0830
0930
1010
1130
1230
1330
1130
1530
1630
1800
1900
2000
210C1
2200
2300
2400
183
182
183
182
18 "1
181
183
183
183
182
184
185
177
180
180
179
136
173
183
180
181
165
173
176
172
177
176
171
173
1 QOf
Down
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
) 4P
_
G.O
G.O
6.0
6.0
6.0
0.8
1.8
3.0
3.0
3.0
*2
3.0
*
3.0
*
6.5
*
5.0
*
5.2
*
3.0
7.0
*
7.0
*
8.3
*
8.0
.pH
Start
NF*
NF
8.0
*
7.2
*
r>.7
*
7.6
7.6
*
7.6
*
7.5
*
7.0
*
7.1
*
6.9
*
6.9
7.0
*
7.2
*
7.3
*
7.1
ppm
up at
NF
550
725
1100
1200
1250
1300
1100
900
975
900
90(1
850
650
900
925
900
925
f,50
500
NF
1000
1000
900
875
925
900
900
900
NOX
ppm
2010
NF
460
440
440
440
460
450
380
380
380
400
420
420
420
460
460
380
420
400
400
NT
420
380
400
•400
400
370
400
400
C02
%

NF
13.0
13.5
13.8
14.0
14.0
15.5
12.0
10.0
11.0
15.0
1M.O
13.5
11.5
1«4.0
16.0
15.5
15.0
NF
NF
Nr
16.5
16.0
15.5
15.0
14.0
16. 0
15.0
17.0
02
%

NF •
7.6
7.6
9.0
9.0
8.4
8.0
9.2
9.8
8.0
NT
NP
NF
MF
NF
NF
Mr
NF
NF
NF
NF
NF
6.6
6.5
6.6
9.0
6.6
6.6
6.6
S02
ppm

NF
180
160
180
280
280
240
310
320
.300
350
320
280
250
125
145
150
NF
115
95
NF
180
130
150
120
130
110
140
135
ULUL,t,l
NOX
ppm

NF
440
440
440
400
420
400
240
320
310
360
380
390
390
420
400
340
NF
390
390
NF
360
375
360
350
370
360
360
360
C02
%

NF
12.0
13.3
13.5
13.5
12.5
13.5
9.0
8.5
11.0
13.5
13.0
13.0
13.0
13.5
15.0
15.0
NF
NF
NF
NF
11.5
13.0
15.0
14.0
12.0
15.0
14.5
15.5
02
-3L

NF
7.8
7.6
>10.0
8.6
8.4
9.0
>10.0
>10.0
9.0
NF
NF
NF
NF
NF
NF
NF
NT
NF
NF
NF
NF
7.9
7.4
7.8
9.0
7.6
7.8
7.6
% SO2
Removal
Efficiency

_
f.7 . 3
77.9
83.H
76.7
77.6
81.5
71.8
64.4
69.2
61.1
64.4
67.1
61.5
86.1
84.3
83.3
-
82.3
81.0
-
82.0
87.0
83.3
86.3
85.9
87.8
84.4
85.0
          1 Sample line leak
          2 Flow problems until 1800
                reading suspect until 1400, 11-15

-------
                                                                        HOURLY DATA
                   Date

                   11-15
 I
OJ
cn
 I
                   11-10

Time
01 00
0200
0300
U400
0501)
0000
0700
0800
0900
1000
lion
1200
1 300
1 400
1500
1 000
1700
1800
J9I10
2000
2100
2200
2300
2400
01(10
0200
0300
0400
0500
0600
0700
0800
Al
MW
105
105
157
107
160
109
171
109
175
180
182
178
178
178
182
J73
170
174
108
178
179
179
179
179
171
174
109
174
175
177
17 3
175
Inlet
inon
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
SS^fefjfe
A P
*
12.2
*
8.0
*
8.0
*
8.0
*1
5.8
*
3.0
*
3.0
*
5.2
*
5.2
*
7.0
*
7.0
*
7.0
*
9.4
*
12.0
*
13.0
*
12. S
pH
0.5
7.2
7.5
7.5
7.5
7.5
7.4
7.4
7.4
6.4
7.3
7.1
7.3
7.0
7..1
7.1
7.0
7.0
7.2
6.9
7.0
7.1
6.9
•7.0
7.1
7.2
7. 3
7.4
7. 4
7.4
7 . 4
7.3
INLET
S02
PPm

900
800
920
1000
910
900
900
700
1150
1300
1100
.1 050
J050
900
900
900
900
800
800
850
800
800
850
800
840
800
900
850
900
900
900
N(JX
PPm
41.0
420
400
425
395
420
440
420
420
440
440
438
420
460
450
420
420
400
400
420
430
430
430
420
430
430
420
430
430
420
430
400
C02
%
10.0
15.5
16.0
10.5
10.5
17.0
17.0
15.8
J5.9
15.5
J5.8
1.5. 3
10.5
11.0
11.0
11.0
11.8
J1.3
11.5
10.5
11.5
13.0
12.5
12.5
13.5
13.5
13.5
13.5
14.0
14.0
J2.5
11.0
02

6.6
6.8
6.4
6.6
5.4
6.2
6.4
6.6
6.4
6.5
6.8
0.9
0.7
6.8
0.7
7.6
6.4
6.2
0.7
6.8
6.8
6.8
7.0
6.8
6.8
0.8
0.8
8.4
0.4
6.6
7.0
7.8
S02
pprn
160
180
160
130
J35
128
125
125
120
250
340
265
240
270
190
190
180
170
160
160
150
130
150
170
140
180
120
110
90
110
100
100
OUTLET
NOX C02
pprn
370
360
390
390
380
390
390
400
400
400
360
360
360
290
390
400
360
350
360
380
400
400
400
390
420
418
'400
420
420
420
410
400
JL
15.0
14.5
15.0
15.5
15.8
16.0
16.0
J5.4
15.5
14.3
13.4
13.2
14.5
10.0
11. I
10.5
11.0
11.0
10.5
9.8
10.5
12.5
12.0
12.0
12.5
12.5
12.0
13.0
14.0
12.5
J2.5
H.5
02
% S<>2
Removal
% Efficiency
7.4
7.8
8.0
7.8
7.4
7.8
7.6
7.5
7.6
8.0
9.5
8.8
8.8
8.5
7.9
8.0
8.0
8.4
8.2
8.0
8.0
7.8
8.0
7.8
7.8
7.8
7.6
8.0
7.0
7.4
7.2
8.0
82.2 ,
80.0
80.0
85.9
80.5
85.9
80.1
86.1
82.9
78.3
73.8
75.8
77. 1
74.3
78.9
78.9
80.0
8J.I
80.0
80.0
82.4
83.8
81.3
80.0
82.5
78.6
85.0
87.8
89.4
87.8
88.9
88.9
                               Ceritr.i Fugo rc-pair 0940

-------
                                       HOURLY DfeTft
Inlet SCRUBBER
ACFM x 2nd Stage S02
Date
1.1-16
(Contd)





11-17
11-18
11-19







11-20










Time
0900
1000
1100-1800
1900
2000
2100
2135
MW i nnn
17 'i NF
175 NF
180 NF
177 NF
178 NF
179 NF

A P
*
11.5
*
*
1.2
*
0
pH ppm
7.] 850
* 1 NF
* 2 NF
7 . 4 1000
7 . 4 1000
7.4 1 000
Scrubber
INLET
NOX C02
ppm %
•120
•100
NF
'100
380
120
down;
6.5
NF
NF
13.0
9.5
10.0
02
JL
6.5
NF
NF
7.0
7.4
8.0
S02
ppm
70
NF
NF
250
230
210
OUTLET
NOX C02 02
ppny
'400
390
NF
260
290
300
JL JL
9.0 7.8
NF NF
NF NF
9.5 10.0
7.5 10.0
8.5 10.0
% S02
Removal
Efficiency
91.8
_
-
7S.O
77.0
79.0
pinch valve ruptured
Scrubber Down
Scrubber Down
1740
1800
1900
2000
2100
2200
2300
2400
0100
0200
0300
0400
0500
0600
0700
0800
0900
1000
1100
174 *
173 NF
173 NF
182 NF
170 NF
173 NF
174 NF
174 NF
174 JJp
175 g£
173 NF
176 NF
174 NF
175 NF
177 NF
175 NF
174 NF
175 NF
170 NF

*
*
*
*
9.5
*
7.0
*
9.2
*
*
*
*
*
10.0
*
*
*
Scrubber
* 3 300
* 200
7.3 NF
* 800
7.1 7SO
* 800
6.8 800
* 800
7.1 800
800
800
800
800
800
7.2 800
* 950
6.9 1000
* 1100
start
450
4'IU
NF
460
4GO
460
460
460
440
440
440
430
440
430
440
410
•120
380
up
13.5
13.8
NF
1M.O
14.5
1M.O
m.o
13.5
I'l.O
1U.O
I'l.O
14.0
14.0
14.5
11.5
14.5
15.1
20.5

10.0
7.0
NF
7.0
6.8
6.8
6.4
6.4
6.4
6.2
6.2
6.2
6.2
6.4
6.8
6.0
6.0
4.0

220
150
NF
130
100
90
100
150
120
150
90
90
90
120
175
110
120
135

430
420
MF
420
430
400
400
380
380
380
380
380
390
400
400
380
370
370

13.5 6.8
I'l.O 7.0
NF NF
13.0 7.6
14.0 7.8
13.5 8.2
13.5 8.2
12.5 8.2
13.0 8.2
13.0 8.0
13.5 8.0
13.5 8.0
13.5 8.2
14.0 8.0
14.0 7.8
14.1 7.1
15.2 7.2
Ifl.G 702

26.7
25.0
-
83.8
86.7
88.8
87.5
81.3
85.0
81.3
88.6
88.8
88.8
85.0
78.1
88.4
88.0
87.7
Centrifuge diverted 1230 - 13.30
Analyzers having flow problems
Faulty solenoid valve on Inlet sampling line

-------
                                                                     HOURLY DATA
                  Date

                  11-20
                  (Contd)
                  11-21
 I
CO
Time

1200
1 I'll)
1400
1 500
J 000
1700
18 00
1900
2000
2.1 00
2200
2300
2400

OHIO
0200
(HOO
0400
0500
0000
0700
0800
0900
1000
1100
1200
1300
1400
1500
1600
Inlet
ACFM x
MW 1000
173
173
171
173
180
184
177
180
1.7 S
175
17 S
17 S
17 S
173
176
174
172
160
160
160
102
183
177
177
177
182
178
175
177
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
SF
NF
NF
NF
NF
NF
NF
NF
SCRUBBER
2nd
-AP
8.0
*
8.5
*
1.0.0
*
*
*2
*
*
*
*
*3
*4
7.2
*
7.2
*
7.2
*
' 8.9
*
10.2
*
11.7
*
1 1.4
*
10.0
Stage
pH
7.1
7.2
7.1
7.1
7. I
7.0
7.0
7.0
7.0
7.0
7.0
7.2
7.1
7.0
7.0
('.8
0.9
7.0
7.1
7.1
7.2
7.2
7.1
7.1
7.1
7.1
7.0
7.0
7.0
S02
ppm
1100
1000
Nr
1050
1.0 SO
1010
1000
Nr
1100
iioo
1100
900
Nr
1150
1100
1100
1100
1200
1100
1100
950
990
875
875
900
900
950
900
900
INLET
NO*
ppm
400
400
400
410
450
420
420
420
410
4.10
420
400
*
420
420
420
420
190
400
400
410
440
400
450
460
460
450
160
160
C02

18. S1'
12.5
12.0
12. S
12.0
12.5
12.5
11.5
32.5
12.0
12.5
12.5
Nr
Nr
Nr
Nr
11.0
11.0
9.5
10.0
10.5
10.0
10. 5
12.0
12.0
12.5
12.5
12.5
12.5
02
%
6.0
6.0
0.0
5.8
S.S
0.4
6.6
6.0
6.2
6.4
0.2
6.6
6.0
S.S
S.S
6.0
6.0
0.0
5.8
6.0
6.0
6.6
6.6
6.2
5.8
6.4
6.0
6.0
6.0
S02
ppm
140
ISO
Nrl
165
140
140
160
Nr
180
180
170
160
Nr
190
190
240
240
260
240
230
200
160
ISO
155
160
170
175
165
180
OUTLET
NOX
PPm
350
340
380
400
410
400
400
400
400
400
380
390
*
380
380
380
380
340
360
380
370
420
130
410
418
430
430
430
430
C02
%
21. H"
8.5
11.0
10. S
11. 5
9.5
10.5
.10.0
11.0
11.4
1.2.8
12.5
NT
Nr
Nr
Nr
10.0
9.5
10.5
10.5
10. S
11.0
11. S
12.0
12.5
11. S
12.0
11.5
1.1.5
02
%
7.0
8.2
7.0
7.0
7.2
8.4
7.4
7.0
7.2
7.0
6.8
7.0
7.0
7.8
7.8
7.2
7.0
6.8
7.0
7.0
7.0
7.0
7.2
7.0
6.8
6.9
6.8
6.8
7.0
  % S02
 Removal
Efficiency

   87. 3
   85.0

   84. 3
   86.7
   86. 1
   84.0

   83.6
   83.0
   84. S
   82.2
   83
   82
   78
   78
   78
   78
   79
   78
   83.8
   82.9
   82. 1
   82.2
   81.1
   81.6
   81.7
   80.0
                            1 SOg Analyzer maintenance
                            2 SOj Analyzer maintenance
                            ^ 303 Ana.lyzor maintcMiaiicc
                            '* C02 Analyzer malfunction

-------
                                                                    HOURLY DATA
                  Date

                  11-21
                  (Contd)
                  11-22
                  11-23
                  11-24
                  11-24
 I
03
00
 I
inlet SCRUBBER
ACFM x 2nd Stage
Time
1700
1800
1900
2000
2100
2200
2300
2400

MW 1000
184 . NF
189 NF
188 NF
185 NF
IB 5 ' OFF
183 OFF
170 OFF
174 OFF
3BFR DOWN
SCRUBBER DOWN
0239
0300
0400
0500
0600
0700
0800
0900
1000-1500
1530
1600
1700
1800
1900
2000
2100
2200
2300
2400
Scrubber
148 NF
150 NF
149 NF
147 NF
148 NF
147 NF
*2 NF
4P pH
* 7.0
9.6 7.0
* 7.1
*! 7.0
OFF OFF
OFF OFF
OFF OFF
OFF OFF

Boiler
Start Up
0.5 7.7
2.5 7.7
2.4 7.4
4.2 7.4
4.8 7.4
5.5 7.3
* *
S02
ppm
900
900
920
OFF
OFF
OFF
OFF
OFF

INLET
NOX
ppm
4(40
440
450
OFF
OFF
OFF
OFF
OFF

C02

12.0
12.5
12.5
OFF
OFF
OFF
OFF
OFF

02
%
6.8
7.0
6.8
OFF
OFF
OFF
OFF
OFF

S02
PPm
180
180
185
830
840
840
840
850

OUTLET
NOX
ppm
M20
420
Mil)
480
M80
M20
"420
420

C02

15.5
12.5
13.0
13.0
13.0
12.5
13.0
13.0

02
_2L
6.8
7.0
6.8
6.4
6.4
6.4
6.4
6.«4

% S02
Removal
Efficiency
80.0
80.0
79.9
_
-
-
_
-

Down 2300, tube leak

800
875
810
800
900
900
850

380
440
440
440
460
460
90

11.4
12.4
11.5
11.6
12.4
13.4
NF

6.7
6.0
6.8
6.8
5.2
5.4
NF

150
240
250
210
200
190
850

340
too
"420
420
'440
'480
440

9.0.
11.0
10. S
10. M
11. '1
12.5
9.8

8.0
6.8
7.3
7.5
0.9
6.1
7.6

81.3
72. f,
69.1
73.8
77.8
78.9
O
SCRUBBER DOWN
178 NF
178 153. t
178 153.6
178 180.2
180 218.1
180 218.1
169 218.1
178 218.1
181 218.1
156 NF
4.4 7.1
7.0 7.1
7.0 7.0
8.0 7.0
8.0 7.0
9.5 7.2
10.0 7.2
9.4 7.1
9.6 7.0
10. 0 7.0

900
910
900
900
880
900
900
900
900
NF
460
460
450
440
440
460
440
430
430
NF
13.5
1«4.5
13.8
14.0
14.0
13.5
14.0
14.0
14.3
NF
6.4
5.8
6.2
5.9
5.8
6.0
6.0
6.4
6.0
170
160
170
160
160
150
140
160
150
150
380
400
420
•420
(420
440
mo
420
(420
395
12.6
12. U
13.0
12.5
12.8
12.5
13. U
13.0
13.0
13.3
7.0
8.0
7.4
7.0
7.2
7.4
6.8
7.0
7.0
6.1
-
82.2
81.3
82.2
82.2
83.0
84.4
82.2
83.3
83.3
                            1  Trailer sampling outlet  only. Scrubber down mt 2000
                            2  Scrubber down 0855, problem with bushing on screw c'onveyor
                            3  Scrubber start up,  Inlet flow problem*

-------
                                                                       HOURLY DATA
                     Date
                     11-25
 I
W
vo
 I
                     Jl-20


Inlet
SCRUBBER
ACFM x 2nd
Time
01 00
0200
0:100
0>IOO
0500
0000
07 00
0800
OfJOO
1000
1 100
1200
1300
I'lOO
1500
ir.oo
1700
1800
1900
2000
2100
2200
2300
2400
0100
0200
0300
O'lOO
0500
0000
0700
0800
MW
151
152
1.51
1'I7
150
153
1.70
170
182
182
183
181
183
180
182
182
180
181
180
179
181
180
180
173
180
180
181
175
175
109
180
179
1000
207.4
82.9
91.1
91.1
146.4
180.2
173.1
140. C
165.9
188.4
197.6
197.6
197.6
197.6
197. C
197.6
197.6
165.9
NF
165.9
165. S
155. S
153.6
159.7
159.7
159.7
159.7
165.9
165.9
165.9
165.9
165.9
4I_
9.0
2.'l
2.4
2.4
5.0
7.0
6.8
0.0
0.5
8.5
8.5
8.5
8.5
8.5
8.8
9.0
'J.I
'J.I
9.1
9.1
9.1
9.1
9.2
8.8
9.0
9.0
10.0
9.5
9.5
9.5
9.0
9.0
Stage
plj_
7.2
7.3
7.3
7. '4
7.3
7.2
6.9
_
7.1
7.0
_
7.0
7.1
7.1
7.1
7.2
7.1
7.1
7.0
7.0
7.0
0.9
7.0
7.0
7.1
7.1
7.1
7.1
7.1
7.1
7.3
7.2
S02
PPm
910
925
900
900
900
900
900
880
900
990
880
850
900
820
880
900
800
900
850
850
800
775
750
810
900
900
900
900
875
900
NI'2
NP
INLET
NOX
PPm
i|i|0
'130
440
'HlO
440
"WO
M60
l|i)0
1480
480
•480
'180
480
"400
450
'400
MOO
'100
'400
'400
"400
IIGO
'460
'4'40
470
470
400
440
450
450
NT
NF
C02
%
14.0
13.5
13.8
13.8
14.2
14.5
14. 0
12.8
11.8
13.2
13.5
13.5
13.4
13.5
12.2
13.2
14.0
14.0
13.0
13.5
13.9
13.8
13.8
13.4
13.4
13.0
13.0
13.0
13.4
13.0
NP
NP
02
%
5.3
0.4
6.4
r..5
5.9
5.7
0.2
0.2
0.4
O.I
0.0
0.1
0.2
0.4
0.2
0.5
0.4
0.4
7.0
0.4
0.6
G.6
6.0
0.6
0.8
0.9
6.9
0.5
0.8
0.8
NF
NF
S02
ppm
170
245
255
255
220
190
190
185
190
165
175
180
170
165
185
120
150
NFl
NF
130
140
150
160
120
140
140
120
140
150
135
110
120
OUTLET
NOX
PPm
380
340
'350
340
380
390
400
390
420
420
430
420
430
410
420
350
420
NF
NF
420
410
400
400
400
420
420
440
410
400
410
430
430
C02
%
10.5
11.2
11.2
11.0
12.2
12.3
12.4
U.2
11.0
11.9
12.2
13.4
11.3
13.2
13.4
7.03
12.4
NF
NF
12.5
12.4
12.0
12.0
12.2
12.2
12.0
11.9
11.9
12.4
12.0
12.0
12.4
02
%
8.7
8.8
8.9
9.1
8.0
7.0
7.2
7.8
7.6
7.6
7.0
7.6
7.6
7.8
7.7"
G.ti
7.8
NF
NF
7.6
6.6
7.6
8.0
7.8
7.8
8.0
7.8
7.9
7.7
7.9
8.0
7.8
% S02
Removal
Efficiency
8.1.3
73.5
71.7
71 .7
75.0
78.9
78.9
"79.0
80.8
83.3
80.1
78.8
81.1
79.9
79.0
80.7
82.0
-
-
84.7
82.5
80.0
78.7
85.2
84.4
84.4
86.7
84.4
82.9
85.0
-
-
                               J Probo cLcanpil
                               2 Restriction in sampln line

                               ^ CO,  Analyzer  malfunction

-------
                                                                       HOURLY DATA
 I

M
O


Date
11-20.
(Contd)














11-27











Time
0900
1000
1100
1200
1300
I'lOO
1500
1000
1700
1800
1900
2000
2100
2200
2300
2'IOO
OHIO
0200
0300
0'400
0500-1200
1300
1400
1500
1600
1700


MW
182
1.81
179
180
181
179
182
182
182
182
182
180
179
179
181
179
182
182
178
183
180
178
178
170
181
177
Tnloh
ACFH X
1000
165.9
165.9
159.7
165.9
NF
165.9
159.7
159.7
159.7
165.9
173.1
165.9
159.7
159.7
165.9
165.9
NF2
401.4
401.4
401.4
NF3
159.7
153.6
159.7
153.6
146.4
eK-mjnnc-p INLET
2nd
^ P
9.0
'J.O
9.0
9.0
*1
9.'l
9.2
8.9
8.9
9.0
9.2
9.0
8.0
9.0
9.0
9.0
9.0
9.0
9.0
9.0
9.0
9.0
9.0
9.0
9.0
9.0
Stage
pH
7.2
7.1
7.0
7.0
*
6.8
7.0
7.0
6.9
7.0
7.0
7.0
7.0
7.0
7.0
7.0
6 .9
7.0
7.1
7.1
7.1
7.1
7.0
7.0
7.1
*
S02

NF
900
900
900
NF
9 MO
900
1000
1000
950
1000
1000
1000
760
800
800
Nl'2
980
900
875
NF3
NF1*
NF
NT
NF^
NT
NOX
ppm
NF
460
'* SO
'ISO
NF
'ISO
'160
•460
•160
190
•(80
'ISO
500
«*MO
'ISO
'|i|0
NF
'160
•430
M30
NF
NF
NF
NF
NF
NF
C02

Nl
1U.I4
13. "4
13.3
NF
13.6
13.6
13.7
13.8
13.6
13.0
1'*.0
I1*. 2
i"4.8
13.4
1U. 2
NF
1'».2
12.0
12.5
NF
NF
NF
NF
NF
NF
02

NF
6.2
6.8
6.6
NF
6.2
6.8
6.8
6.1*
6.8
6.6
6.7
6.7
6.9
6.8
6.6
NF
6.8
6.8
6.8
NF
NF
NF
NF
NF
NF
S02
ppm
150
150
170
150
I'lO
1'45
165
182
155
165
180
195
185
120
1'I5
1U5
NF
l'*5
130
120
NF
160
173
170
170
170
UUTLtT % S02
NOX
ppm
it'll)
i*i*0
'*20
M30
i*30
'130
U20
•*30
M20
'430
•41*0
•120
•ISO
•420
•430
•120
NF
'130
MOO
MOO
NF
400
NF
NF
NF
NF
C02
%
12.3
12. 'I
12. '1
12. '1
12.6
12.0
12.7
12.8
12.8
12.8
12.5
13.0
13.3
13.7
13.'l
12.8
NF
13.1
11.8
11.8
NF
12. •*
12.'*
12.5
12.6
12.0
Oj
%
7.9
7.9
7.9
7.9
7.8
7.9
7.6
7.6
7.6
7.9
7.9
7.9
7.7
_
7.8
7.8
NF
7.6
7.8
7.6
NF
NF
NF
NF
NF
NF
Removal
Efficiency
_
83. 3
81. 1
83. H

8U.6
81.7
81.8
8'4. 5
82.6
82.0
HO. 5
81. S
8M.2
81.9
81.9
_
8S.2
85.6
86.3
_
-
-
-
-
-
                                Outlet S<>2 Wrt tosting
                              ^ Clean sample linos
                              3 t\imp out on trailer  sampling  system
                              '' Insufficient flow for inlet,  NO,, and Oj  readings
                                Coal feeder problems

-------
                                                   HOURLY DATA
Date

1 1-28
H-29
11-30
12-1

Time

Inlet
ACFM x
MW 10QO
SCRUBBER
2nd Stage
4P pll
Nil DATA TAKKN - TIIANKSIil VJNC,
NO DATA TAKF.N - TIIANKSKlVTNi;
O'lOO1
1000
1.100
1201)
1300
1400
1 500
1600
170(1
1800
1900
2000
2100
2200
2300
2401)
0100
0200
0300
0400
0500
0600
0700
0800
0900
1000
HOO
1200
180
175
108
172
182
182
182
181
176
170
178
178
170
175
175
176
177
172
174
1.78
174
178
179
177
179
177
170
179
197.6
197.6
228.4
NF2
NF
NF
228.4
218.1
242.2
242.2
228.4
242.2
242.2
NF2
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
215
215
NF
NF
S.2
0.7
*
5. 5
*
6.5
0.8
6.4
6.8
0.7
0.0
0.8
0.8
*
*3
*
*
6.0
*
6.5
*
6.5
*
6.5
*
6. 5
*
6.5
6.8-
7 . 4
*
7.0
*
7.0
7.0
7.1
0.9
7.0
7.0
7.0
7.0
*
*
*
*
7.0
*
0.9
*
7.0
*
7.0
*
7.0
*
7.1
S02
ppm
INLET
NOX
ppm
C02
HOMDAY .
02
%

S02
ppm

OUTLET
NOX
ppm

C02

02

HOLIDAY
950
1000
970
900
Nl'
NF
1000
1010
1000
1.000
1000
1010
1010
900
900
900
900
900
Nr
Nr
Nr
NT
Nr
Nr
1000
1000
900
900
420
450
440
Np2
Nr
NF
440
450
460
400
420
400
470
450
455
440
440
400
Nr
Nr
Nr
Nr
Nr
NF
440
440
'180
400
12.8
1.3.1
13.4
Nr
13. 3
13.5
13.0
12.9
13.5
13.5
13.5
13.3
13.5
13.2
13.2
13.3
13.2
Nr1'
NF
Nr
Nr
NF
Nr
Nr
12.9
13.4
12.0
12.6
6.8
7.0
6.7
Nr
7.0
6.8
7.0
7.0
6.9
6.7
0.8
7.0
0.7
0.8
Nr
Nr
Nr
Nr
NT
Nr
Nr
Nr
NF
NF
6.6
6.5
6.4
6.3
240
240
220
250
Nr
Nr
150
160
165
170
185
185
185
160
160
160
160
160
Nr
Nr
Nr
NF
NF
Nr
200
200
200
200
390
390
400
Nl'
NF
NF
410
410
410
410
400
410
410
410
405
400
400
415
NF
NF
NF
NF
NF
NF
400
400
405
405
12.0
12.0
12.0
NF
12.0
12.0
11.0
11.0
12.0
12.1
12.0
12. I
12.0
12.0
12.0
J2.0
12.0
NF
NF
NF
Nr
w
Nr
Nr
11.9
11.8
11.4
11.4
8.5
8.5
H 2
NF
8.0
8.0
8.0
8.0
7.5
7.8
8.0
8.0
8.0
7.9
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
8.1
7.9
7.5
7.5
          1 lie-nan at 0900 afti>r holiday
          2 rlow problems
          ^ 02 Recordor down
          '• Flow probJ cms nut il O')00
 Removal
Efficiency
                                                                                                   74.7
                                                                                                   76.0
                                                                                                   77. 1
                                                                                                   72.2
                                                                                                   85.0
                                                                                                   84.2
                                                                                                   83.5
                                                                                                   83.0
                                                                                                   8)
                                                                                                   81
                                                                                                   81
                                                                                                   82
                                                                                                   82
   82.2

   82.2
   82.2
                                                                                                  80.0
                                                                                                  80.0
                                                                                                  77.8
                                                                                                  77.8

-------
                                                                    HOURLY DATA
inlet JjCKUBBER
Date
12-1
(Contd)






Time
1300
1401)
1500
1 600
1700
1800
1900
2000
2050
MW
179
179
168
180
178
178
176
177
183
ACFM >
NF
NF
NF
NF
NF
NF
NF
NF
NF
4P
*
0.5
*
6.0
*
0.2
*
5.4
*1
stage
pH
*
7.1
*
7.1
*
7.1
A
7.1
*
S02
ppm
900
900
900
900
900
900
900
900
900
INLbT
NOx
ppm
450
450
440
440
450
440
435
450
500
C02
12.3
12.3
12.6
12.6
12.5
12.3
12.3
12.0
12.2
02
_2L
6.3
6.3
6.2
6.2
6.3
6.3
6.2
6.5
>10.0
S02
ppm
200
260
18U
200
210
210
210
210
210
OUTL
NOX
ppm
405
MOO
'400
390
405
400
400
400
MOO
ET
C02
11.2
11.1
11. 1
10.8
U.3
11.1
11. 1
10.6
NF
02
7.6
7.6
7.3
7.6
7.M
7.5
7.5
7.7
6.3
% S02
Removal
Efficiency
77. R
71.1
80.0
77.8
76.7
76.7
76.7
76.7
76.7
 I
CO
H-
N)
                 12-2

                 12-3

                 12-M

                 12-5
                 12-6
SCRUBBER DOWN
SCRUBBER
SCRUBBER
17002
1800
190(1
2000
2100
2200
2300
2400
moo
0200
0300
0400
0500
0600
0700
0800
0900
1000
1100
1200
1300
165
167
173
175
175
174
177
175
179
182
178
176
176
178
178
180
180
180
180
180
178
DOWN
DOWN
51.2
56.3
58.9
110.1
110.1
105.0
179.2
165.9
179.2
179.2
179.2
179.2
117.8
179.2
230.4
197.1
240.6
240.6
240.6
230.4
240.6


0.8
0.8
2.8
2.8
4.5
3.3
5.2
4.8
5.0
5.0
5.0
5.0
M.O
•4.5
M.O
0.3
8.2
8.0
8.0
8.0
8.5


7.1
7.1
7.2
7.1
7.2
7.2
7.1
7.2
7.0
7.0
7.0
6.9
7.2
7.2
7.2
7.0
7.0
7.0
7.0
7.0V
7.1


900
950
-940
910
950
950
900
950
950
1000
1000
1000
950
1000
900
900
990
990
900
930
1000


430
'420
425
'130
425
440
425
460
'420
430
420
420
400
420
400
440
460
460
470
* 390
460


14.8
14.9
14.3
14.4
15.0
15.0
15.3
15.2
15.0
l't.8
15.2
1M.5
15.0
15.2
15.0
15.0
13.8
13.8
13.7
13.6
l't.5


7.0
7.2
7.4
7.2
6.8
5.8
6.0
6.6
6.0
6.0
6.2
5.6
7.2
6.4
6.6
6.6
6.8
6.8
6.9
7.0^
6.8


230
228
250
250
220
280
230
230
220
220
230
240
230
225
160
155
210
170
160
145
450


385
380
410
420
420
420
440
400
380
400
380
400
340
350
360
400
410
450
460
; 360
420


13.0
13.1
12.5
13.5
15.4
15.0
15.0
13.5
13.0
13.0
12.0
14.0
12.0
13.0
14.0
14.0
12.5
13.5
13.5
12.5
13. S


8.5
8.4
7.8
7.9
7.0
5.8
7.1
8.2
8.6
8.6
9.0
7.4
9.6
9.0
9.0
8.8
8.0
7.M
7.5
8.0
7.3


71.4
76.0
73.4
72.5
76. 8
7CI.S
7 '4 . 'I
75.8
76.8
78. 0
77.0
76.0
75.8
77.5
82.2
82.8
78.8
82.8
82.2
84.4
SS.O
                             Scrubber down 20SO, Irak in scrubber bleed lines
                             Scrubber  start up

-------
                                                                    HOURLY DATA
OJ
 I


Inlet
ACFM x
Date Time
12-6 1400
(conttl) 1500
1000
1700
1800
1900
2000
2100
2200
2300
2400
12-7 0100
0200
0300
0400
0500
0000
0700
0800
0900
1000
1100
12002
1300
1400
1500
1000
1700
1800
1900
2000
2100
MW
179
175
180
178
178
172
179
178
176
177
179
177
170
170
170
170
170
170
173
173
176
179
179
179
179
175
180
177
177
178
179
177
1000
240.6
207.4
197.6
165.9
188.4
180.2
180.2
180.2
188.4
188.4
188.4
288.4
228.4
228.4
228.4
228.4
228.4
228.4
207.4
207.4
207.4
135.7
140. B
146.4
173.1
*3
NF
188.4
188.4
188.4
188.4
197.6
SCRUBBER
2nd
A P
8.5
8.5
8.5
8.8
9.0
8.5
8.5
8.9
8.5
8.6
8.5
9.0
9.0
9.0
9.0
9.5
9.5
9.5
9.5
9.5
9.5
7.0
3.0
5.0
7.5
*3
*
8.0
8.8
8.6
8.6
8.6
Stage
pH
7.0
7.1
7.1
7.0
7.0
7.0
7.1
7.1
7.1
7.1
7.1
7.1
7.1
7.1
7.1
7.1
7.2
7.2
7.2
7.1
7.1
7.0
7.5
7.4
7.3
*
*
7.0
7.1
7.1
7.1
7.0
SO2
ppm
1000
1000
1000
1000
1000
1000
1000
1000
800
880
850
850
900
920
900
900
900
900
800
900
800
800
890
11.40
875
NT
NF
960
1020
980
1020
1020
INLET
NOx
PPm
400
400
450
400
460
460
460
400
430
440
440
440
430
430
440
440
440
440
4 '40
460
440
420
420
NF
420
NF
NF
425
440
440
430
440
CC>2
%
14.5
14.3
13.8
14.2
14.0
13.8
14.0
14.2
14.3
14.0
14.0
14.0
14.0
13.5
14.0
13.5
13.5
13.5
14.0
14.0
13.5
13.5
13.3
NF
14.5
NF.
NF
13.4
12.9
13.1
12.9
12.7
02
%
0.8
6.8
6.8
6.6
0.6
0.8
0.0
0.5
6.6
6.6
6.6
6.4
0.4
0.4
0.4
0.6
6.6
6.4
6.6
6.5
0.8
0.8
7.0
NF
6.7
NF
NF
6.8
6.7
6.6
6.6
6.6
S02
ppm
NT1
150
170
168
200
208
165
160
170
180
180
170
175
190
175
180
180
170
150
150
150
150
230
252
120
NF
NF
210
190
145
115
135
OUTLET
NOx
ppm
NF
420
410
420
415
410
420
420
400
410
410
420
390
400
400
420
420
410
420
430
410
400
400
380
390
NF
NF
380
400
400
400
395
C02
JL
NF
12.5
12.6
12.5
12.5
13.0
12.6
12.1
13.0
12.7
13.0
13.0
13.0
12.5
12.5
12.5
12.5
12.7
12.8
12.8
12.8
12.5
12.2
13.0
12.5
NF
NF
12.2
11.8
12.0
12.2
12.4
02

NF
8.0
7.8
8.0
8.0
7.8
7.8
7.6
7.8
7.8
7.8
7.8
7.8
8.0
7.8
7.6
7.6
7.6
7.6
7.6
7.6
7.8
8.3
8.2
8.2
NF
NF
7.4
7.4
7.3
7.4
7.2
% 502
Removal
Efficiency
.
85.0
83.0
83.2
80.0
79.2
83.5
84.0
78.8
79.5
78.8
80.0
80.0
79.3
80.0
80.0
80.0
81.1
81.3
83.3
82.6
81.3
74.2
77.9
86.3
_ .
_
78.1
81.4
85.2
88.7
86.8
                             Outlet probe cleaned
                            2 1st  Stage outage, leak  in recycle header
                            3 F\imp outage on  sampling ay Stem

-------
                                                                   HOURLY DATA
                 Date

                 12-7
                 (oontd)

                 12-8
tB
M
*>.
 I
                 12-9


Inlet
ACFM x
Time
2200
2300
2UOO
0100
0200
0300
OMOO
0500
OOOO2
0700
0800
0900
1000
1100
1200
1300
I'lOO
1500
1000
1700
1800
1900
2000
2100
2200
2300
2MOO
01(10
0200
0300
OMOO
HW
175
176
179
181
179
179
180
180
180
179
177
IMft
l'IU
1M3
137
129
110
111
106
102
103
96
97
102
102
100
102
101
101
101
101
1000
188 .
188.
188.
188.
188.
NF
188.
188.
188.4
188.4
188.4
188.4
180.2
180.2
173.1
165.3
165.9
146.4
146.4
153.6
153.6
180.2
188.4
188.4
188.4
188.4
188.4
188.4
188.4
188.4
138.4
SCRUBBER
2nd
AP
8.8
8.G
8.G
8.5
*1
*
8.5
8. 5
8.5
fl.5
fl.5
8.3
8.1
8.1
7.3
0.0
6.2
3.5
3.5
3.8
5.6
3.8
3.9
3.9
3.5
3.8
'l.O
'1.2
'I.')
4.4
4.4
Stage
pll
7.0
6.9
7.0
7.0
*
*
7.1
7.0
7.0
G.9
r,.8
fi.7
r..9
6.9
6.9
0.9
ft. 9
f>.9
7.2
7.0
7.0
7.0
7.L
7.1
7.2
7.2
7.0
7.0
7.0
7.0
7.0
S02
ppm
1000
1000
1000
900
1000
NF
1000
1000
1000
950
1000
12110
1100
1200
1100
1200
1100
1100
1.050
1050
1020
1020
1020
1100
1000
1050
1100
1200
1200
1200
1200
INLET
NOX
ppm
MGO
U50
UUO
1,1,0
U50
NF
UMO
i|50
M80
'ISO
M60
M10
"100
MOO
U20
"120
"120
MOO
MOO
M10
M20
MM5
M30
M20
MOO
380
410
MHO
MMO
4MO
, 420
C02
%
13.0
13.1
13.0
13.0
13.0
NF
13.0
13.0
13.0
13.0
13.2
13.0
13.0
12.6
12.5
13.0
NF
12.5
12.7
13.0
12.0
12.7
12. H
11.7
12.7
11.5
13.0
13.0
13.0
13.0
13.0
02
%
6.M
O.M
6.2
6.6
6.6
NF
6.2
0.2
6.2
6.2
0.2
0.2
6.0
5.8
5.8
6.M
NF
6.5
7.0
6.2
7.8
7.0
6.M
7.2
6.6
8.0
6.4
6.0
6.4
6.6
6.6
S02
ppm
1MO
1M5
1MO
140
NF
NF
150
150
135
140
180
200
200
200
220
2MO
220
240
250
250
260
260
270
280
240
280
290
290
280
290
280
OUTLET
NOX
ppm
MOO
"*00
MOO
MOO
NF
NF
330
MOO
t|l|Q
I'll)
MOO
MOO
360
360
360
380
360
360
3MO
380
MOO
MOO
390
390
380
360
360
MOO
400
400
380
C02
%
12. 3
11.8
12.0
12.5
NF
NF
12.0
12.0
12.0
12.5
12.2
12.2
12.0
12.0
12.5
12.0
12.7
12.3
11.0
10.5
10.6
10.5
11. 1
10.0
11.3
11.4
11.5
12.2
12.5
12.0
11.7
02
%
7.4
7.4
7.2
7.4
NF
NF
7.6
7.6
7.6
7.4
7.0
7.2
7.0
7.0
6.8
7.0
6.8
8.0
8.M
8.9
9.0
8.9
8.4
9.0
8.M
fl.M
8.0
7.M
7.6
7.8
7.8
  % S02
 Removal
Efficiency

   86.0
   85.5
   86.0

   SU. M
   85.0
   85.0
   8(>. 5
   85.3
   82.0
   83.3
   81.8
   83. 3
   80.0
   80.0
   80.11
   78.2
   76.2
   76.2
   7H.5
   7'I. 5
   73.5
   7«l.5
   76.0
   73.3
   73.0
   75.8
   76.7
   75.8
   76.7
                             Outlet probe blocked
                           2 Drop in load, wet coal

-------
                                                                    HOURLY DATA
                  Date

                  12-9
                  (rontd)
CO
                  12-10


Time
0000
0000
07(M)J
0800
0900
1000
1100
1200
1.300
1400
1SOO
loon
1700
1800
L900
2000
2100
2200
2300
2400
0100
0200
0300
0400
0500
0600
0700
0800
0900
1000
1100
1200


MW
110
10J
100
9 9
101
IBS
IBS
185
105
170
172
LO')
182
190
189
l')3
182
183
1.75
173
176
174
164
148
147
174
156
LSI
178
183
184
180
Inlet
ACFM x
1000
188.4
188.4
188.4
188.4
197.6
197.6
197.6
218.1
218.1
218.1
207.4
207.4
207.4
218.1
228.4
218.1
228.4
228.4
228.4
228.4
228.4
228.4
228.4
242.2
228.4
228.4
228.4
228.4
228.4
228.4
218.1
173.1
SCRUBBER
Zna
AP
4.2
4.4
'l.'l
'1.3
4. 5
'l!s
1.3
4.7
5.8
5.8
5.1
4.0
5.8
S.7
6.2
0.0
6.0
6.2
6.2
5.8
6.0
6.0
6.0
7.0
7.0
6.5
7.0
6.8
5.4
'1.8
3.8
2.2
Stage
pll
7.0
7.0
7.1
7.1
7.1
7.0 ,
6.9
6.9
6.8
7.0
7.1
7.1
7.0
6.9
7.0
7.0
0.9
0.9
6.9
7.2
7.1
7.0
6.8
6.9
6.9
6.9
7.0
7.1
7.1
6.9
6.2
7.2
S02
ppm
1200
1200
1200
1050
1100
900 >
850
850
920
900
900
900
900
900
950
900
920
950
980
980
1000
950
1000
900
850
800
800
800
800
800
800
800
INLET
NOX
PPm
400
440
400
420
380
420
400
410
400
4GO
460
445
440
430
410
420
420
400
420
420
400
360
400
400
380
380
380
400
420
410
400
400
C02
%
13.0
12.0
13.0
13.0
13.2
12.5
12.5
12.8
12.5
12.8
13.0
12.7
12.9
13.3
13.6
13.4
13.2
13.5
13.8
12.5
14.0
13.5
14.0
13.5
12.5
13.5
13.5
I'l. 3
l't.3
13.7
14. 3
12i7
02
X
6.4
7.0
7.0
0.8
6.M
7.2 ;
7.3
6.0
7.0
0.0
6.4
6.6
6.6
6.4
6.4
6.4
6.4
6!4
0.0
6.8
5.2
6.4
5.8
6.2
7.5
6.5
6.5
6.0
6.4
6.8
6.2
7.0
S02
ppm
310
310
320
220
230
220 \
185
175
190
185
200
195
175
190
180
220
225
280
290
180
190
220
230
240
220
200
200
170
150
200
240
230
OUTLET
NOX
ppm
380
380
360
380
320
370
360
380
420
400
400
370
400
400
380
380
370
360
390
380
380
350
380
370
360
340
.340
360
370
380
380
320
C02
%
12.5
13.0
11.5
12.5
12.5
11.0
12.2
11.5
12.0
13.0
12.8
11.0
11.2
11.8
11.9
11.6
12.1
12.0
12.5
12.0
12.0
12.5
12.5
13.0
11.0
13.0
12.5
12.0
12.3
12.3
12.0
10.0
02

7.2
6.9
8.4
7.3
6.8
8.7
8.4
8.4
8.0
6.8
6.9
8.2
8.0
7.7
7.8
8.2
7.6
7.4
7.2
7.6
7.8
7.5
7.5
6.8
8.8
7.4
7.6
7.8
7.8
7.8
8.0
>10.0
  % SO 2
 Removal
Efficiency
   74.2
   7'I. 2
   73.3
   79.0
   79.1.
   75.6
   78.2
   79.M
   79.3
   79.4
   77.8
   78.3
   80.6
   78.9
   81. I
   75.6
   75.5
   70.5
   70.4
   81.6

   8J.O
   76.8
   77.0
   73.3
   74.1
   75.0
   75.0
   78.8
   81.3
   75.0
   70.0
   71.3
                            1 Rising Boiler load

-------
                                                                      HOURLY DATA
 I
CO



Inlet
ACFM x
Date
12-10
(fontd)







12-11




12-12

12-13






Time
1300-1600
1700
1800
190(1
200(1
2100
2200
2300
2UOO
0100
0200
0300
O'lOO2
0500^
HIM)'1
1 UOO
J8101'
1900
2000
2100
2200
2300
2<400
MW
17 S
170
170
178
177
177
160
108
153
10"!
102
1 (>2
1.03
103
170
172
120
118
111
116
113
108
107
1000
NF
207.4
207.4
207.4
207.4
218.1
228.4
228.4
228.4
242.2
242.2
242.2
180.2
180.2
197.6
197.6
228.4
228.4
242.2
228.4
242.2
242.2
228.4
SCRUBBER
2nd
A?
*1
M.'l
't.O
M.O
'4.2
"4. '1
5". 5
5.6
6.0
6.0
6.0
6.0
1.0
0
'4.0
0
1.'4
3!2
2.7
2.7
5.3
5.0
5.2
Stage
pll
7.3
7.1
6.9
7.0
7.0
7.0
7.0
7.0
7.0
7.0
6.9
6.9
7.2
7.1
7.2
7.1
7.2
7.2
7.1
7.1
0.8
7.1
7.1
S02
ppm
NF
980
1020
1050
1090
1100
1120
1100
1100
1100
1100
1100
1100
1100
1200
MTS
1250
1250
1180
1200
1250
1200
1100
INLET
NOX
ppm
Nr
IIMO
M30
M20
"100
MOO
510
UOO
380
uno
'400
"400
•4in
300
380
Nr
395
390
390
mo
•100
•42(1
•450
C02

NF
13. M
13.3
12. '1
13.0
13.3
1U.5
13.1
13.5
13.5
13.2
13.5
13.0
11.0
1H.6
NT
15.0
I'l.O
13.9
13.3
13.6
13.8
1.3.14
02

NF
6.2
6.6
7.0
6.8
6.2
5.«4
6.3
6.0
6.0
G.2
6.2
7.0
9.0 '
6.5
NF
5.0
5.7
5.5
3.2
6.2
6.0
6.3
SO 2
ppm
NF
225
230
235
2UO
2>45
260
220
220
220
2'IO
220

>lf)00
305
308
55
285
290
275
235
225
210
OUTLET
NOX
ppm
NF
390
360
350
360
360
370
360
360
360
390
390
360
1420
360
360
90
320
320
320
350
380
390
C02
%
NF
10.0
12.3
11.2
11. '4
12. 3
12.6
12.1
12.0
12.0
13.5
12.5
12.0
12.5
16.1
10.9
3.2 >
11.5
11.6
10.7
13. M
13.6
12.6
02

NF
8.9
7.8
8.G
8.7
7.8
7.G
7.7
7.8
7.8
6.6
7.2
8. "4
7.0
5.G
6.7
•10.0
8.8
8.0
8.7
7.6
7.U
7.8
% 502
Removal
Efficiency

77.0
77.5
77.6
78.11
77.7
70.8
81.8
81.8
81.8
78.2
8.1.8
78.2
-
7 "1.0
-
95.0
77.2
75.'4
77.1
81.2
81.3
80.9
                               Pump out on sampling apparatus
                             2 1st Stage outage, dropprd hammer
                             3 Scrubber shut clown - O'l25
                             ** Scrubber start up - 1230
                             5 Sciiibber slint down - 1'I20
                             c Scrubber start up - 1810

-------
                                                                    HOURLY DATA
                  Date
                  12-14
 I
CO
                  12-15


Inlet
ACFM x
Time
0100
0200
037)0"^
" 0400
0500
0600
0700
0800
0900
1000
1100
1200
1300
14001
1500
1600
1700
1800
0100
0200-1300
1400
1500
1600
1700
1800
1900
2000
2100
2200
2300
2400
MW
102
100
101
102
102
102
1(12
102
101
103
121
133
135
135
140
140
144
147
140
*3
175
170
178
179
176
178
135
151
168
172
173
10QP
153.0
153.6
153.0
153.0
153.6
153.0
153.6
153.0
159.7
146.4
159.7
159.7
165.9
159.7
153.6
120.3
153.6
153.6
165.9
*
159.7
159.7
140.8
188.4
197.6
197.6
140.8
140.8
140.8
159.7
159.7
SCRUBBER
2nd
4JL
5.3
5.4
5.4
5.3
5.3
5.3
5.3
5.5
5.5
0.4
6.5
6.5
0.2
6.2
0.0
2.4
*2
*
7.2
*
6.7
6.5
6.5
0.5
8.2
7.3
0.0
8.0
7.0
7.0
6.7
Stage
pH
7.2
7.1
7.1
7.0
7.0
7.0
7.1
7.1
7.1
7.2
7.1
7.1
7.1
7.0
7.0
7.1
*
*
7.1
*
7.0
7.0
6.9
7.0
7.0
7.0
6.8
7.0
7.0
7.0
7.0
S02
ppm
11.00
1100

-------
                                                                    HOURLY DATA
 I
CD
M
00
 I


Inlet
ACFM x
Date Time
12-16 0100
0200
0300
0400
0500
0600
07 OU
0800
0900
loon
1100
12001
1300
1MOO
1500
16002
1700
1800
1900
2000
2100
2200
2300
2400
12-17 0100
0200
^s^^OSne^
	 omno
0500
MW
155
172
170
15(1
1S5
171
168
160
145
143
145

146
146
143
140
140
140
142
142
140
138
1 MO
145
156
160
160
160
160
1000
159.7
130.6
159.7
153.6
153.6
140.8
146.4
146.4
140.8
140.8
153.6
159.7
74.8
74.8
82.9
74. B
140.8
140.8
165.9
165.9
165.9
165.9
165.9
165.9
159.7
159.7
159.7
159.7
159.7
SCRUBBER
2 iid
j& P
6.5
6 .0
7.0
fi.2
6.0
6.0
6.0
6.0
6.5
O.I
6.3
6.4
0
0
0
1.8
6.0
5.4
8.2
8.2
8.2
8.3
8.4
8.4
7.8
7.5
7.5
7.5
7.5
Stage
pll
7.0
7.1
7.1
7.0
7.1
7.2
7.3
7.3
7.3
7.3
7.2
7.2
7.5
y 8
>8
7.5
7.1
7.1
6.9
6.9
7.0
7.1
7.1
7.1
7.1
7.1
7.2 (
7.1
7.2
SOa
ppm
1040
10MO
1000
1000
1000
1100
moo
1000
885
850
800
940
890
885
900
770
800
790
780
860
840
800
840
820
820
840

800 •
800
INLCT
NOX
ppm
390
420
M10
380
MOO
MOO
400
MOO
380
370
380
370
350
3M5
350
360
360 "
370
360
360
360
380
380
380
380
380
380
380
380
C02

14.0
14.8
14.8
13.2
13.8
14.8
14.8
14.0
13.8
13.8
13.7
14.0
13.6
14.0
13.9
14.0
14.0
12.0
13.5
14.5
12.5
14.0
15.5
12.5
13.4
14..0
13.5
14.5
13.5
02
%
6.8
6.2
6.8
7.8
7.0
6.4
6.8
6.2
5.8
5.7
5.8
5.7
6.0
6.0
6.0
6.4
6. 4
7.3
6.4
6.2
6.4
6.0
5.9
6.5
6.8
6.2
6.501
6.2
6.6
S02
ppm
185
200
200
210
190
200
180
150
140
150
175
160
685
680
135
150
140
140
140
120
130
140
140
130
120
120
13 tr
130
120
OUTLET
NOX
ppm
360
390
380
340
330
360
330
350
340
340
350
350
320
320
210
260
260
340
320
330
340
340
325
325
340
340
340
340
340
C02
%
12.0
12.6
12.2
13.4
14.2
13.5
11.5
13.0
12.0
12.5
12.7
13.8
12.9
12.5
9.5
11.0
11.5
13.0
13.0
12.5
11.5
11.7
13.5
12.5
12.5
12.5
12.5
12.5
12.5
02

8.0
7.8
8.4
7.5
7.5
7.8
8.4
8.0
7.2
7.2
6.4
6.2
7.0
6.5
10.8
9.4
7.8
7.2
7.4
7.2
7.2
7.4
7.0
7.8
7.8
8.0
7.5
7.5
7.8
% S02
Removal
Efficiency
82.2
80.8
80.0
79.0
81. 0
81.8
82.0
85.0
R'1.2
82.4
78.1
83.0
23.0
23.2
85.0
80.5
82.5
82.3
82.1
86.0
84.5
82.5
83. 3
84.1
85.4
85.7
83.8
83.8
85.0
                            1 Scrubber 2nd Stage out for repairs
                            2 Coal feeder problems - Unit #3

-------
                                                                  HOURLY DATA
W
Date
12-17
(oontd)
















12-18








Time
0000
07 OO1
0800
090H2
1000
1100
1200
1300
1400
1500
1600
1700
1800
1900
2000
2100
2200
2300
2400
0100
0200
0300
0400
05003
0600
0700
0800
0900
1000
1100
MW
160
158
145
151
162
174
182
182
182
181
182
181
180
181
163
174
180
182
182
174
188
190
190
190
185
190
172
175
174
174
Inlet
ACFM x
10QO
159.7
159.7
95.2
130.0
159.7
159.7
180.2
197. C
180.2
165.9
165.9
180.2
180.2
188.4
197.6
197. C
197. C
188.4
180.2
188.4
188.4
188.4
IBS. 4
138.4
138.4
138.4
XF ^
.)F
SCRUBBER
2nd Stage
AP pH
7.8
7.H
1.1
3.7
8.2
8.7
0.0
8.5
9.7
"J.8
10.0
10.1
10.1
10.3
12.0
10.1
10.0
10.1
10.0
10.5
9.8
9.8
9.8
9.8
10.2
10.5
9.5
9.8
0.8
9.8
7.2
7.1
7.3
7.2
7.1
7.0
7.1
7.1
7.2
7.1
7.1
7.2
7.0
7.1
7.0
7.0
7.1
7.1
7.0
7.0
7.1
7.1
7.1
7.2
7.0
7.0
7.0
7.1
0.9
6.9
S02
ppm
800
840
780
790
1050
950
960
810
790
800
800
840
800
800
800
800
800
900
950
950
930
900
930
900
1080
1020
1100
1020
1020
1140
INLET
NOX C02
ppm %
380 13.2
380 12.5
320
380
365
395
470
460
460
MOO
M65
400
420
410
MOO
M05
MOO
MMO
MOO
420
440
460
'480
460
460
450
440
MMO
M40
450
.13.8
14. 0
11.8
13.0
13.6
12.7
13.5
13.5
14.5
14.0
13.5
14.5
14.5
1M.5
14.5
14.0
14.0
14.0
14.2
14.2
14.8
14.4
14.4
14.2
15.0
15.5
14.5
14.5
02
JL
6.8
6.8
6.2
6.5
6.4
6.8
6.1
6.5
6.3
6.4
5.9
5.2
5.9
6.0
5.8
5.8
5.8
5.6
3.6
5.4
5.6
5.6
5.6
5.6
5.6
5.8
5.0
5.0
5.4
5.4
S02
ppm
110
140
200
165
170
135
180
135
110
102
120
110
120
110
120
125
125
100
170
160
150
160
150
138
174
174
186
168
204
192
OUTLET
NOX C02
ppm %
340 12.2
340 12.1
340
345
340
380 ,
440
450
450
410
410
400
390
400
340
380
360
400
380
380
400
400
440
420
410
380
380
MOO
390
400
13.5
13.9
11.9
12.3
12.7
12.9
12.7
12.6
13.0
13.0
13.0
13.0
14.0
14.0
13.0
11.5
12.0
13.0
12.7
12.7
13.7
13.5
14.0
13.5
15.0
14.0
13.0
13.0
02
JL
7.8
7.8
6.0
6.7
7.8
7.2
7.0
6.7
6.7
7.4
6.4
6.8
5.0
6.4
5.4
6.8
5.2
6.8
6.8
6.6
7.0
6.8
6.5
6.5
6.5
6.5
6.6
5.6
6.4
6.4
% S02
Removal
Efficiency
80.3
83.3
7M.4
79. J
83.8
85.8
81.3
83.3
86.1
87.3
85.0
80.9
85.0
86.3
85.0
84.4
84.4
88.9
82.1
83.2
83.9
82.2
83.9
84.7
83.9
82.9
83.1
83.5
80.0
83.2
                             Coal feeder problem
                           2 Change liquid flow rate
                           3 SO2 readings from OuPont unit

                           * Testing using inlet ports

-------
                                                                      HOURLY DATA
10
O
I


Date
12-18
(contd)











12-19


„
^













Time
1200
1300
1400
1500
1GOO
1700
1800
J900
2000
2100
2200
2300
2MOO
OJ Ofll
0200
0300
JIUOO
- 0500'
0000
0700
08 OO2
0900
1000
1100
1200
1300-1500
10003
1700
1800


Inlet
ACFM 3:
SCRUBBER
2nd Stage S02
MW 1000 -AP
174
174
174
173
174
173
174
173
171
171
172
172
167
166
166
JOO
160
162
162
158
J57
157
157
156
152

143
150
143
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
188.4
188.4
188.4
188.4
188.4
188.4
197.6
197.6
207.4
159.7
165.9
165.9
SCRUBBR*
173.1
188.4
197.6
7.8
9.0
9.8
9.8
9.8
9.2
9.8
9.0
9.0
8.5
8.0
8.0
8.2
8.2
8.2
8.2
8.5
8.5
8.5
8.5
8.5
8.M
*
*
*
DOWN
2.8
6.0
6.2
pH pprn
7.U 11MO
7.1 11 HO
7.U II'IO
7.0 1200
7.0 11«U)
7.0 ll'lfl
7.0 11"IC
7.0 11«IU
7.0 II'IO
6.9 11MO
7.0 1140
7.0 II'IO
6.9 II'IO
6.9 II'IO
7.0 1140
7.0 II'IO
7.0 12GU
6.9 11UO
7.0 1080
7.0 1080
7.0 1200
7.0 1200
* 1200
* 1200
* 1200
- 2nd Stage
7.0 1200
7.1 1300
7.1 1200
INLET
NOX
Ppm
410
460
440
440
440
MMO
MMO
MMO
MOO
400
MOO
MOO
400
400
400
MOO
'ISO
430
MMO
M20
400
420
460
450
440
recycle
440
420
430
C02
%
12.8
I'l.O
1M.2
14.5
14.0
14.2
13.5
14.2
14.0
14.2
14.0
14.0
13.7
14.5
14.3
14.3
14.5
14.1
14.0
m. 5
!•». 3
15.0
15.0
13.5
14.0
header
13.5
12.0
15.0
02
%
0.8
5.'l
5.4
5.M
5.0
5.5
5.8
5.4
5.8
5.6
5.9
5.6
6.0
5.M
5.5
5.0
5.5
5.M
6.0
5.8
5.8
5.8
5.8
G.2
6.0
had to
5.8
G.O
5.0
S02
OUTLET
NOX
ppm ppin
210
192
192
192
200
200
200
200
200
200
200
210
192
192
192
192
210
204
192
210
400
400
400
390
MOO
MOO
MOO
MOO
360
360
360
360
360
380
360
300
390
380
380
360
234 360
230
300
300
300
be
300
220
228
360
360
350
340
repaired
390
370
380
C02
JL
12.5
12.5
13.2
12.5
12.5
12.5
12.5
12.5
13.0
13.0
13.2
12.3
13.0
12.0
12.0
12.0
12.6
12.9
13.2
12.5
12.5
12.0
11.5
12.0
11.0

12.5
11.0
13.0
02

7.2
6.6
6.4
6.M
6.6
6.8
6.8
6.8
7.0
7.0
6.8
7.0
6.8
7.0
7.0
6.8
6.8
6.8
6.8
6.8
6.8
7.2
8.0
8.0
8.0

7.0
7.6
7,0
% SO2
Removal
Efficiency
8l.fi
83.2
83. 2
RM.O
82.5
82.5
82.5
82.5
82.5
82.5
82.5
81.6
83.2
83.2
83.2
83.2
83.3
82.1
82.2
80.6
80.5
80.8
75.0
75.0
75.0

75.0
83.1
81.0
                             1 SOp readings from DuF'ont unit
                             2 2nd Stage outage (for repairs)
                             3 Scrubber start up

-------
                                                                     HOURLY DATA
 I
03
N>



Inlet
ACFM x
Date
12-19
(contd)




12-20






















Time
1900
2000
2100
2200
2300
2MOO
01001
0200
0300
OMOO
0500
060I)2
0700
0800
0900
1000
1100
1200
1300
1MOO
1SUO
1600"
1700
1800
1900
2000
2100
2200
2300
MW
1MO
IMG
IMS
1M<)
IMS
129
100
100
100
100
100
90
90
99
98
9M
88
90
89
91
89
95
102
102
106
US
12M
128
120
1000
197.6
197.6
197.6
197.6
197.6
197.6
197.6
207.4
207.4
207.4
105.0
105.0
99.3
91.1
99.3
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
95.2
95.2
99.3
95.2
SCRUBBER
2nd
A P
G.M
6.M
6.0
0.0
O.M
3.M
3.6
3.7
3.9
3.5
3.8
3.5
3.5
3.M
3.0
3.0
3.0
3!a
3.8
3.8
3.8
3.8
3.8
3.2
3.0
3.0
3.0
2.8
3.0
Stage
pH
7.1
7.1
7.1
7.1
7.0
7.1
7.2
7.1
7.0
7.0
7.0
7.0
7.0
7.0
' 7.0
7.0
7.0
7.2
7.2
7.2
7.1
7.0
7.0
7.0
7.0
7.0
7.1
7.1
7.1
S02
ppm
1320
1320
1200
1280
1200
1200
11MO
HMO
1180
1200
HMO
1080
1180
1200
1180
1180
1020
900
900
960
'• 930:
' 8 MO ',
. 960
, 8 MO .,
1000
980
1020
980
980
INLET
NOx
ppm
MOD
420
MOO
MOO
M20
MSO
MSO
M.30
M90
M90
M25
.390
MOO
M30
MOO
M70
MOO
M80
MMO
500
'180
M80
MSO
M70
M60
MOO
380
380
380
c<>2

1M.O
12.5
13.0
12.5
13.5
12.8
12. M
.1.2.3
12.5
12. M
12.8
NF
NF-^
NI-
13.5
13. M
12.5
12.5
13.0
13.5
15.0
12.5
1M.O
13.0
13.0
12.5
13.0
12.5
12.5
02
%
6.0
5.8
5.8
6.0
6.1
5.7
6.0
5.2
5.9
5.9
6.2
7.2
6.3
7.2
6.2
6.8
7.0
6.M
6.2
7.1
6.0
6.1
6.0
6.0
6.1
6.2
6.0
6.0
6.0
S02
ppm
210
2MO
238
2MO
2MO
2MO
252
252
282
282
252
255
280
285
2MO
2MO
200
186
192
192
198
190
210
200
2MO
200
200
230
2MO
OUTLET
NOX
ppm
330
370
3MO
300
360
350
370
M05
Ml 5
Ml 5
370
350
380
350
360
370
MOO
M10
390
M20
M20
MOO
M10
360
370
3 MO
3UO
320
320
C02
%
13.0
11.5
11.7
11.5
12.5
11.6
11.8
10.7
11.5
11.3
11.2
NF
NF
NF
13.0
12.2
11.5
11.0
11.5
12.5
1M.O
11.5
12.5
12.0
11.0
11.0
11.0
11.0
11.5
02
%
7.0
7.0
7.0
7.M
7.0
8.0
7.5
6.8
7.0
6.9
7.5
8.5
7.5
8.1
8.1
7.8
8.2
8.2
8.0
7.3
6.3
7.8
7.5
7.2
8.0
8.0
8.0
8.1
7.6
% S02
Removal
Efficiency
83.0
81.8
80.2
8J .3
81.0
80.0
77.9
77.9
70.1
70.5
77.9
70. M
70.3
70.3
79.7
79.7
80. M
80.0
80.0
80.0
78.7
77. M
78.1
76.2
76.0
79.6
80. M
76.5
75.5
                              S02 readings from IhiPont unit
                            2 Cn2 Analyzer not working
                            3 Boiler feed problem wet coal
                            ** S02 readings from TECO unit resumed

-------
                                                                    HOURLY DATA
 I
W




ACFM x
Date
12-20
(contd)
12-21























12-22






Time
2UUO

OlflU
0200
0300
O'lOO
0500
0600
0700
0800
0900
1000
11(10
1200
1300
1400
1500
1600
1700
1800
1900
2000
2100
2200
2300
2400
0100
02UO
0300
0400
0500
0600
0700
MW
130

129
131
131
133
125
122
130
129
131
HI
131
131
132
132
132
132
138
141
144
144
146
147
147
148
149
137
113
111
115
111
110
1000
82.9

105.0
115.2
130.6
135.7
135.7
130.6
125.4
140.8
140.8
NF
NF
NF
NF
NF
NF
NF
NF
NF
125.4
125.4
125.4
125.4
130.6
135.7
130.6
140.8
140.8
140.8
140.8
135.7
135.7

2nd
A P
2.8

4.5
4.5
5.8
0.2
5.8
5.5
5.5
6.4
5.4
6.6
6.0
6.6
6.6
6.6
6.8
6. 4
6.4
6.4
6.4
6.4
6.4
6.4
6.4
6.5
6.7
6.5
6.7
0.7
6.3
6.5
6.8
Stage
pH
7.1

7.0
7.0
7.0
6.9
7.0
7.1
7.1
7.1
7.0
7.0
7.0
6.8
6.9
6.9
6.9
7.1
7.1
7.1
7.1
7.1
7.0
7.1
7.0
7.2
7.2
7.1
7.2
7.2
7.2
7.1
7.1
S02
ppm
720

820
800
840
960
950
940
920
860
860
980
1000
1160
1180
1160
1220
1000
1000
1000
920
1080
1080
1080
1080
920
900
900
1100
1100
940
1080
1000
NOX ~C02
ppm
380

380
375
420
405
420
390
370
375
400
400
400
390
390
300
390
300
300
300
300
280
250
250
230
230
220
215
445
430
370
390
380
5«
12.5

12.0
12.0
13.9
13.5
13.5
14.1
14.4
. 13.5
12.6
13.5
13.5
12.5
13.0
14.5
14.5
13.0
13.0
13.0
13.0
13.0
13.0
14.0
14.0
14.3
13.3
16.4
14.5
14.7
13.7
14.0
14.3
02
%
6.2

7.3
6.3
6.3
6.4
6.8
5.8
5.7
0.0
6.4
6.1
6.4
6.4
6.2
0.2
5.8
6.1
6.1
5.9
6.0
5.8
5.8
5.4
5.6
5.4
6.0
5.4
6.0
6.7
6.6
6.7
6.6
S02
ppm
190

170
160
190
140
160
150
160
110
120
160
160
140
200
200
420
240
240
280
180
200
220
200
200
150
140
120
220
210
190
220
260
OUTLET ">* sn-i
NO^ C02
Ppm
340

340
335
365
380
375
350
350
320
364
300
360
350
300
260
260
260
260
260
260
240
230
220
210
195
195
190
400
370
360
340
360 '
_2L
11.5

11.8
11.7
12.5
12.4
12.3
12.0
12.5
11.0
12.0
12.5
12.5
12.5
13.0
13.5
14.0
12.0
12.5
11.5
12.0
12.5
12.0
13.0
13.0
12.7
12.5
13.8
13.3
13.8
12.7
12.5
13.4
02
%
7.5

7.3
7.4
7.8
7.6
7.5
7.6
7.8
8.4
7.2
7.2
7.0
7.0
7.4
7.6
5.2
7.2
7.2
7.2
7.0
7.0
7.1
7.0
7.0
6.8
7.0
7.7
7.3
7.3
8.3
8.4
7.5
Removal
Efficiency
73.0

79.3
80.0
77.4
85.4
83.2
84.0
82.6
87.2
86.0
83.7
84.0
87.9
83.1
82.8
65.6
76.0
76.0
72.0
80.4
81.5
79.6
81.5
81.5
83.7
84.4
86.7
80.0
80.9
79.8
79.6
74.0

-------
                                                                    HOURLY DATA
 I
to
ro
to
 I
Inlet SCRUBBER

Date
12-22
(rontd)














12-23








12-24
12-25
12-26
ACFM x 2nd
Time MW 1000 Ap
08001 136 135.7 6.2
0900-1000 SCRUBBER OUT
11002 174 140.8 6.2
1200 173 140.8 f'.3
13(10 174 140.8 0.3
1400 175 146.4 7.0
1500 170 146.4 6.2
lf.00 176 146.4 0.6
1700 177 146.4 7.0
1800 17'l 140.8 0.8
1900 179 140.8 f'.M
2000 181 140.8 6.4
2100 180 135.7 0.'4
2200 178 140.8 0.4
2300 170 140.8 <>.'!
2400 100 165.9 8.3
0100 141 NF3 8.8
0200 116 180 2 9.2
0300 108 130*2 9.2
0400 108 188.4 9.2
0500 109 180.2 9.2
0600 110 180.2 8.8
0700 119 180.2 9.0
0800 140 173.1 8.0
0900H 169 146.4 6.2
SCRUBBER DOWN
SCRUBBER DOWN
NO DATA TAKEN - Crew
Stage
_£H_
7.1

7.2
7.2
7.2
7.1
7.2
7.1
7.1
7.1
7.1
7.2
7.2
7.1
7.1
7.0
6.9
6.9
7.0
7.0
7.0
7.0
7.0
7.0
7.2


still
S02
PPm
980

890
800
800
880
800
800
760
800
8HIJ
880
930
840
880
840
NF3
780
840
800
810
850
1000
880
860


INLET
NOX
PPm
400

440
440
400
440
440
440
420
420
400
400
420
400
400
400
NF
400
400
405
400
385
380
360
350


C02
JL_
14.0

12.5
12.5
13.5
14.5
13.0
J2.5
12.5
12.5
13.0
13.0
13.0
13.0
13.0
13.0
NF
13.0
13.5
13.0
13.5
12.6
13.0
12.5
12.0


02
JL
6.0

OJ8
6.8
6.5
0.4
0.8
6.8
7.0
7.0
7.0
7.0
7.0
7.0
6.8
6.9
NF
7.3
7.2
7.2
7.2
8.0
7.0
6.8
7.2


S02
PPm
180

128
140
200
200
200
100
160
160
200
200
220
200
210
140
NF
150
150
100
140
160
160
160
160


OUTLET % SOp
NOX
pprn
360

'390
390
380
380
380
380
380
360
360
360
360
360
360
360
NF
380
380
380
375
340
340
320
320


C02
JL
12.5

12.6
12.0
13.0
12.5
13.5
11.5
11.0
11.5
11.5
11.0
11.0
12.0
11.5
12.0
NF
12.0
12.0
12.4
12.5
12.0
13.0
12.0
11.0


02
JL
7.6

8.1
8.1
8.0
8.0
8.0
8.1
8.5
8.2
8.1
8.5
8.6
8.4
8.2
8.2
NF
8.4
8.2
8.2
8.0
8.4
7.0
7.8
8.2


Removal
Efficiency
81.0

85.6
82.5
75.0
77.3
75.0
80.0
78.9
80.0
77.3
77. 1
76.3
70.2
76.1
83.3
-
80.7
82.1
80.0
82.7
81.2
84.0
81.8
81.4


on holiday
                             Sorubber down to repair leaks
                           ^ Scrubber start up
                           3 Plugged sample line
                           ** Sombber shut down - repair leaks

-------
                                                                           i«X)RLY DATA
                     Date

                     12-27
 I
CO
NJ
it*
 I
                    12-28
Inlet SCRUBBER
ACFM x 2nd
Time
08 HO1
0900
JOOO
1100
1200
1300
J400
1500
1600
1700
1800
1900
2000
2100
2200
2300
2400
oinn
0201)
0300
0400
0500
0600
0700
0800
0900
1000
1100
J200
1300
1400
1500
MW
1M2
174
177
179
1RI
179
177
17 S
175
172
171
172
172
180
179
17 f,
174
17 S
175
135
135
134
134
158
109
174
170
167
16 M
164
103
138
1000 AP
180.2 6.0
180.2 5.6
NF 5.4
NF 5.7
NF 5 i|
NF 7^
NF g.O
NF 9.0
228.4 8.7
228.4 9.3
228.4 g.s
228.4 9.5
228.4 9^5
218.1 8.8
228.4 9.3
228.4 9.3
228.4 9.3
228.4 9.3
228.4 9.3
242.2 10.2
242.2 10.2
242.2 10.2
242.2 10.2
218.1 9.8
228.4 10.0
228. 9.6
228. 10.1
228. 10.0
228. 10.1
228. JO.O
228.4 10.0
228.4 11.0
Stage
pH
7.0
7.0
7.1
7.1
7.1
7.2
7.1
7.0
7.0
7.0
7.1
7.0
7.0
7.1
7.1
7.1
7.0
7.0
7.1
7.0
7.0
6.9
6.9
7.0
7.0
6.8
7.0
7.0
7.0
7.1
7.1
7.0

S02
ppm
1000
108 U
960
960
1040
1040
960
960
940
920
900
900
900
860
800
870
880
860
820
920
920
920
960
1100
1160
1160
1120
1080
1180
1020
loon
1160
INLET
NOX
PPm
460
480
480
480
480
460
460
460
430
430
435
430
440
440
470
440
450
450
440
450
450
440
440
440
4'40
440
440
380
350
370
380
370
C02
%
13.8
13.0
14.0
14. U
14.0
13.0
14.0
14.0
12.8
13.4
13.2
13.5
13.3
13.0
14.3
14.2
14.5
14.2
14.2
13.4
14.5
14.2
14.4
14.3
14.3
14.3
14.0
14.0
14.0
14.0
14.0
15.0
02

5.2
6.4
6.0
G.O
G.O
7.0
6.0
G.O
6.4
G.O
6.3
6.3
6.3
6.6
6.2
6.9
5.8
6.2
6.2
6.5
6.2
6.2
6.0
6.4
6.2
6.0
6.0
G.I
6.0
6.0
6.0
5.0

S02
PPm
160
240
200
200
180
240
200
200
120
130
110
100
110
110
110
80
80
70
70
80
100
80
90
100
160
140
120
220
240
120
140
120
OUTLET
NOX

420
420
420
420
420
420
380
380
410
370
380
385
400
400
420
405
410
410
400
420
400
400
400
400
•400
410
380
350
320
340
360
360
CU2
%
12.0
12.0
11.5
11.5
11.3
12.5
13.0
13.0
11.5
12.8
12.4
12.0
12.1
12.4
12.8
12.9
12.8
13.8
13.6
13.4
14.0
13.4
13.4
13.8
13.5
13.0
13.3
13.0
13.0
13.0
13.0
12.5

02
%
8.0
8.0
8.4
8.5
8.0
8.0
6.0
6.2
7.8
7.0
7.6
7.5
7.4
7.3
7.4
7.4
7.4
7.0
7.0
6.5
7.0
7.0
7.0
6.8
7.0
7.2
7.2
7.0
7.0
7.0
7.1
7.8
% S02
Removal
Efficiency
84.0
77.8
79.2
79.2
82.7
76.9
79.2
79.2
87.2
85.9
87.8
88.9
87.8
87.2
86.3
90.8
90.9
91.9
91.5
91.3
89.3
91.3
89.5
90.9
86.2
87.9
89.3
79.6
79.7
89.2
80. 0
89.7
                               *• Crr-w began talcing data

-------
                                                                    HOURLY DATA
 I
CO
to
(Jl
 I
Inlet SCRUBBER

Date
12-28
(contri)







12-29

















12-3U
12-31

Time
IfiOO1
1700
1800
1900
2000
2100
2200
2300
2400
0100
0200
0300
O'ino
osoo
(16002
0700
0800
0900
1000
1100
1200
1300
moo
1500
1000
17 OO3
1800

MW
135
172
172
179
176
179
178
176
13'l
135
135
135
135
135
135
135
ll'l
102
101
101
127
156
1S7
145
137
148
153
SCRUBBER
SCRUBBER
ACFM x <*nd
IflJlfl. 4JL.
242.2 11.0
228.4 9.6
228.4 9.8
228.4 9.0
228.4 9.0
228.4 9.5
242.2 0.6
242.2 *».6
266.2 10.0
255.0 9.8
255.0 10.0
255.0 10.2
255.0 10.2
255.0 10.2
255.0 10.2
255.0 10.2
266.2 11.0
266.2 10.4
228.4 3.3
153.6 3.3
146.4 3.6
159.7 3.0
146.4 2.8
159.7 2.6
165.9 3.5
130.6 0
130.6 0
IX)WN
DOWN
Stage
pll
7.0
7.0
7.0
7.0
7.1
7.1
7.0
7.0
7.0
6.9
6.9
6.9
6.9
6.9
6.9
7.0
7.0
7.0
7.3
7.2
7.0
6.9
7.0
6.9
7.1
7.7
*


S02
ppm
1020
1000
960
960
940
1000
1050
10SO
1020
1080
1020
1020
1020
1080
1080
1080
1020
920
1200
1300
1340
1240
1520
1520
1680
200
200


INLET
NOX
ppm
3.90
380
WO
400
400
395
390
385
390
UOO •
'100
iMIO
440
440
420
380
370
300
360
3 MO
350
380
380
370
370
270
190


C02
JL_
114.0
13.7
].i|. 5
lit. 6
13.9
13.9
1U.3
I'l.O
13.8
13.8
14.0
1U.8
14.8
14.8
1'l.fl
15.0
I'l.O
13.0
12.5
12.5
I'l.O
13.0
13.0
13.3
13.2
10.2
7.1


02
_2L
0.6
6.0
0.0
0.1
0.2
0.2
5.9
0.2
0.8
6.7
6.0
0.0
0.0
6.0
0.0
5.8
7.0
7.2
8.0
7.2
6.5
0.8
6.2
0.0
5.5
8.<4
10.0


S02
ppm
108
132
120
120
130
138
132
144
144
138
132
120
126
132
138
132
128
16"4
144
210
300
280
320
300
300
1600
*


OUTLET
NOX
PPm
300
350
370
370
380
370
365
355
370
380
360
mo
400
'100
400
380
340
330
320
290
310
310
320
320
330
380
*


C02
JL
13.1
12.9
13.3
13.4
12.8
12.5
13.4
13.3
13.3
13.0
13.8
13.5
14.2
14.2
13.8
14.0
12.5
11.5
12.0
11.0
11.0
11.0
11.5
12.0
11.4
12.5
*


02
JL
7.4
7.4
7.4
7.2
7.4
7.2
7.0
7.0
7.0
7.5
6.8
7.0
6.8
6.8
7.0
6.8
8.0
8.5
8.5
9.0
9.0
8.8
8.4
8.0
7.8
6.8
*


% S02
Removal
Efficiency
89. 'I
86.8
86.9
87.5
80.2
80.2
87. '1
86.3
8S.9
87.2
87.1
87.0
87.0
87.8
87.2
87.8
87.0
82.2
89.0
82.4
77.0
77.4
78.9
70.3
82.1

-


                             Readings for SO-, after 1000 arc from IhiPont unit
                           2  Boiler cut to three coal  feeders, 0000-1300
                           3  Scrubber down at 1645, leak in olbow

-------
                                                                     HOURLY DATA
Time
   Inlet
  ACFM x
MW 1000.
 SCRUBBER
 2nd Stage
.AP    pH
                                                            S02
                                                            ppm
                                        INLET
                                      NOX    C02
                                      pptn     %
02    S02
       OUTLET
      NOX   C02
      PPM    %
                                                                              02
               % 502
              Removal
             Efficiency
 I
01
to
                  l-'l
                  1-5
                  1-6
                  1-7
                  1-8
             DOWN
    SCRUBBER DOWN
         ScrubbcT operating with  1st  stage only
21001   171  266.2   0    OFF  900     'I'lO    1U.2
22002   171  266.2   0    OFF  840     120    II.8

    SCRUBBER DOWN -  1st Stage off line  at 0835
    SCRUBBER IK)WN
    SCRUBBER IK1WN
                                                                                5.8
                                                                                5.8
960
835
                                                                  WO
                                                                  1420
1U.8
1M.8
                                                                      5.8
                                                                      5.8
                                                                      0
                                                                     .0
1735
2000
2100
2200
2300
2'400
0100-0200
0300
O'lOO
0500
0600
0700
0800
0900
1000
1100
1200
1300
1100
1st
183
179
178
182
180
*'l
183
181
180
177
175
178
182
178
176
181
180
181
Stage only
121-8
loo . z
279.6
266. 2
266.2
266.2
*
266.2
266.2
266.2
266.2
266.2
266.2
266.2
266.2
266.2
266.2
266.2
120.3
3.3
3.5
3.5
3.i|
3.1
*
0
0
0
0
0
0
0
0
0
0
0
0

OEF NF3
OFF NF
OEF NF
OFF 1080
OFF 1120
* NF
OFF 1080
OFF 1120
OFF 1120
OFF 1120
OFF 1160
OFF 1280
OFF 1280
OFF 12'40
OFF 1210
OFF 1350
OFF 1350
OFF H80

420
375
350
370
720
NF
680
620
620
620
620
5HO
130
'410
110
100
370
390

12.6
13.0
12.7
12.5
13.5
NE
13.0
13.0
14. 0
13.5
1'4.0
12.5
13.8
13.5
13.5
13.8
1'4. 5
1'4.0

7.2
f>. 5
7.2
7.0
6.8
NF
6.8
7.0
6. *4
6.8
C.2
7.2
6.5
5.8
5.8
5.9
5.9
6.2

NF
NE
NE
1000
NF
NE
NF^
9GO
1080
1080
1080
1120
1160
11'40
1200
1200
1210
1290

390
320
3>40
380
670
NE
NF
600
600
600
590
520
•420
•400
370
390
360
380

12.8
13.2
13.1
12.8
NE
NF
NF
12.0
13.0
13.0
14.0
12.5
13.8
13. S
11.2
14.0
I'l.O
13.6

7.2
8.6
8.0
7.0
NF
NF
NF
8.0
7. '4
7.«
6.1
7.14
6.8
6.2
6.M
6.2
6.1
6.2

-
_
_
7. "I
-
-
_
1<4.3
3.6
3.6
6.9
12.5
9.M
8.1
3.2
11. 1
10. «4
6.5
                              Trailer on line
                            2 Trailer off linn due to pump failure
                            •j Trailer on line; SOp TBCO unit down
                            * Sample line repair
                            5 First Stage only operating

-------
                                                                    HOURLY DATA
 I
0)

Date Time
1-8

Inlet
ACFM x
MW 1000

(oontd) 1405-1600
17001
1800
1900
2000
2100
2200
2300
2400
1-9 01002
0200
0300
0400
0500
0600
0700
0800
0900
1000
1100
1200
1300
1400
1500
1600
1700
1800
1900
2000
2100
2200
2300
2400
176
179
179
181
180
183
*
*
184
183
184
184
178
179
179
179
170
154
154
149
149
149
149
147
140
130
133
128
125
126
129
124

SCRUBBER
2nd
AP

Stage

First Stage down
180.2
255.0
291.8
291.8
291.8
291.8
291.8
438.3
291.8
291.8
266.2
291.8
291.8
291.8
291.8
291.8
291.8
291.8
291,8
291.8
291.8
291.8
291.8
291,8
266.2
291.8
291.8
291.8
291.8
266.2
266.2
266.2
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
OFF
OFF
OFF
OFF
OFF
OFF
OFF
OFF
OFF
OFF
OFF
OFF
OFF
OFF
OFF
OFF
OFF
OFF
OFF
OFF
OFF
OFF
OFF
OFF
OFF
OFF
OFF
OFF
OFF
OFF
OFF
OFF
S02

INLET
NOX
Ppm

C02

02
%

S02
ppm

OUTLET
NOX
ppm

C02
_*_

02

% S02
Removal
Efficiency

for repairs
1300
1320
1300
1380
1390
1390
1430
1430
1300
1400
1390
1390
1500
1360
1300
1300
1070
1080
1080
1050
980
900
900
780
750
790
710
710
840
820
800
810
380
375
380
355
350
345
330
330
300
300
300
280
280
280
240
245
420
420
420
450
440
440
460
460
520
470
450
500
400
460
440
480
14.2
12.6
12.7
13.4
14.1
13.5
13.6
. 13.5
13.0
13.0
13.2
13.0
12.2
13.5
13.8
13.8
13.8
13.8
13.8
13.0
13.5
13.2
13.4
13.3
12.1
11.8
12.2
12.2
13.8
13.3
12.5
13.0
6.4
5.8
5.8
5.8
5.4
5.5
5.3
5.5
5.2
5.2
5.4
5.4
5.6
5.4
5.4
5.4
5.6
5.8
5.8
5.5
5.4
5.6
5.8
5.7
6.5
7.0
0.5
6.0
5.3
5.6
5.9
6.0
1220
1290
1290
1340
1260
1280
1340
1340
1300
1380
1360
1360
1380
1300
1300
1200
990
950
900
900
900
850
BOO
720
620
710
680
630
730
730
740
730
370
375
350
350
340
335
320
320
300
280
280
280
280
260
240
220
410
410
410
440
420
420
440
440
400
470
440
SOO
455
420
430
460
12.4
12.3
14.0
12.4
12.5
13.2
13.0
13.0
13.0
12.8
13.0
12.8
12.0
13.5
13.5
12.5
13.8
13.5
13.2
13.0
13.2
13.2
13.4
12.8
12.8
12.3
12.3
11. '»
11.8
12.0
12.4
12.0
6.5
6.2
5.6
6.0
5.9
6.0
5.8
6.0
5.8
6.1
6.0
6.0
6.0
6.0
6.0
6.0
6.1
5.8
5.8
5.8
5.4
5.8
5.8
5.8
5.6
6.5
6.2
7.4
6.8
6.7
6.4
7.0
6.2
2.3
2.3
2.9
9.4
7.9
6.3
6.3
0.0
1.4
2.2
2.2
8.0
4.4
0.0
7.7
7.5
12.0
16.7
14.3
8.2
5.6
11. 1
7.7
17.3
10.1
'1.2
11.3
13.1
8.2
7.5
9.9
                           1 First Stage only on line
                           2 First Stage only operating

-------
                                                                  HOURLY DATA
                Date

                1-10
                1-11
 I
00
tsi
00
 I
                1-12


Time
moo
0200
0300
0400
0500
0000
0700
0800
0830
1340
1400
1500
1000
1700
1800
1900
2000
2100
2200
2300
2400
01 OO1
0200
0300
0400
0500
0600
0700
0800
0900
1000


MW
120
119
119
119
119
119
119
119
Inlet
ACFM x
1000
266.2
266.2
266.2
266.2
242.2
242.2
266; 2
266.2
SCRUBBER
2nd Stage SO2
AP pH ppm
0 OFF Bin
0 OFF 800
o OFF sno
0 OFF 800
0 OFF 800
0 OFF 8 00
0 OFF 800
0 OFF 900
Complete scrubber shut
Complete scrubber start
174
178
177
169
179
177
176
176
177
17 S
135
12S
125
126
126
127
114
108
109
109
119
146.4
180.2
197.6
197.6
197.6
140.8
197.6
197.6
197.6
218.1
218.1
218.1
242.2
242.2
218.1
218.1
218.1
207.4
207.4
207.4
197.6
1.5 7.8 1100
2.5 7.9 1100
5.0 7.4 NF
4.0 f..9 1000
5.5 7.0 1000
3.2 7.2 990
0.0 7.2 1000
6.6 7.1 1000
6.0 7.0 1000
6.0 6.9 1000
7.2 7.1 1140
7.2 7.0 1100
7.4 6.9 1100
7.4 7.0 1200
7.4 7.1 1J40
7.4 7.0 1140
6.3 7.2 1100
6.3 7.1 900
5.8 7.1 1080
O.'l 6.9 1080
6.2 7.0 1420
INLET
NOX
ppm
390
460
460
460
440
440
440
440
clown
up
410
430
450
450
450
440
440
420
440
440
440
450
440
450
450
440
410
400
420
420
430
C02

13.8
13.4
13.0
1.3.0
13. '1 '
13!'»
13.4
13.8


12.5
14.4
14.2
13.0
13.0
J3.0
14.0
in. 2
14.2
in. 3
13.5
14.0
14. 0
J4.0
13.6
13.0
13.5
13.5
14.2
13.5
1"4.0
02
%
6.0
0.4
6.6
6.6
6.4
6.4
6.2
6.0


6.8
5.8
5.0
6.2
6.2
7.0
6.2
6.4
6.4
6.4
6.0
6.0
6.2
6.0
6.4
6.5
6.6
6.4
6.4
6.4
5.8
S02
PPm
760
770
720
720
720
720
720
800


340
240
NF
140
140
180
170
120
120
120
140
140
140
160 ,
135
130
145
130
150
280
230
OUTLET % Sf>2
NOX
ppm
450
440
440
440
470
420
420
440


380
390
450
440
•440
400
400
380
380
380
380
•410
410
420
110
410
380
385
380
390
380
C02
%
J 3 . 4
12.8
13.0
12.8
12.8
13.0
13.4
13.5


13.4
12.8
11.4
13.0
13.0
11.5
13.5
13.0
13.5
13.0
13.0
12.5
12.6
12.5
13.0
12.5
12.0
12.4
12.4
13.2
13.1
02
JL
6.8
7.0
6.8
7.0
6.8
6.8
6.8
6.8


6.8
7.8
6.8
6.8
6.8
8.0
6.8
7.2
7.2
7.8
7.8
7.2
7.0
7.2
7.U
7.2
7.8
7.8
7.5
7.5
7.2
Removal
Efficiency
0.2
3.8
10. 0
10. n
10.0
10.0
10.0
11.1


69.1
7fl.2
_
86.0
8C.O
8.1.8
83.0
88.0
88.0
88.0
87.7
87.1
87.3
86.7
88.2
88.6
86. 8
85.6
80.1
7"4.1
«3.8
                            Coal  feeder problems

-------
                                                                           HOURLY  DATA
 I
to
ro
vo
 I


Inlet
ACFM x
Date Time
1-12 1100
(contcl) 1200
1300
1400
ISOO
1000
1700
1800
1900
2000
2100
2200
2300
2MOO
1-13 0100
0200
0300
0400
0500
0600
0700
0800
O'JOO
1000
1100
1200
1300
1400
ISOO
1600
1700
1800
1900
2000
MW
127
127
129
131
132
131
133
J33
133
133
133
133
132
125
118
120
119
119
119
120
124
127
130
128
128
129
129
128
129
128
129
129
130
128
1000
197.6
197.6
197.6
188.4
188.4
197.6
197.6
197.6
197.6
218.1
207.4
207.4
218.1
207.4
207.4
197.6
207.4
207.4
207.4
207.
207.
207.
207.
207.
207.4
207.4
197. C
197.6
197.6
207.4
207.4
207.4
207.4
207.4
SCRUBBER
2nd
AP
6.5
6.1
6.0
6.0
6.0
6.0
G.O
6.0
6.0
G.O
0.0
0.0
0.0
0.0
0.2
0.2
0.2
0.2
6.2
6.4
6.0
6.2
5.8
6.1
6.3
6.2
6.2
6.5
6.5
6.0
6.4
0.6
6.6
6.6
Stage
pH
7.0
7.0
7.0
7.1
7.1
7.1
7.1
7.1
7.2
7.2
7.2
7.1
7.1
7.1
6.9
7.1
7.1
7.1
7.1
7.1
7.1
7.2
7.2
7.3
7.2
7.1
7.2
7.2
7.1
7.1
7.0
7.0
7.0
7.0
S02
ppm
1580
1580
1000
1640
1040
1600
1500
1400
1400
1500
1450
1400
1380
1380
1400
1350
1300
1300
1300
1300
1400
1300
1150
1100
1050
1000
1000
1000
1000
1000
1000
1000
1000
1000
INLET
NOX
ppm
420
425
420
425
400
410
400
400
400
400
400
395
380
380
390
390
380
380
380
380
380
380
370
380
3flS
380
380
380
390
380
390
390
380
420
C02
_2L_
13.5
14.6
14.0
.14.6
13.4
14.5
14.5
14.5
14.5
14.5
14.5
14.5
14.5
14.0
12.5
13.0
13.5
13.5
13.0
13.5
13.7
14.4
14.3
14.1
13.2
13.7
14.3
14.1
13.8
14.3
14.5
14.0
14.5
14.5
02

6.3
5.9
5.8
5.6
6.0
5.8
6.0
6.0
6.0.
5.8
5.8
5.8
S.8
6.2
6.5
6.3
0.2
0.2
6.2
6.0
5.8
5.6
5.6
5.6
5.5
5.6
5.5
5.5
5.8
5.5
5.5
5.7
5.5
5.5

S02
ppm
270
200
260
200
270
280
226
250
250
270
270
250
250
250
250
250
230
240
230
230
240
245
235
210
200
205
175
150
140
160
170
130
175
150
OUTLET
NOX
ppm
390
390
380
380
370
370
370
370
380
380
380
340
340
340
340
340
350
370
340
330
340
340
340
330
340
340
340
340
340
340
3 SO
340
350
370
C02
%
12.8
13.1
13.2
13.5
12.8
13.5
12.5
12.5
12.5
12.5
13.0
12.5
12.5
12.0
11.5
11.5
12.0
12.5
11.8
12.5
12.5
13.0
12.5
12.5
12.3
12.2
12.5
13.0
12.8
12.8
13.0
12.7
13.0
13.2

02
_*_
7.0
7.0
7.2
6.8
7.2
7.0
7.2
7.2
7.0
7.0
7.0
7.0
7.0
7.2
7.6
7.6
7.3
7.2
7.3
7.0
6.8
6.8
7.0
6.8
6.7
7.0
6.8
7.1
7.2
7.1
7.0
7.2
7.0
7.0
% S02
n 1 '
Removal
Efficiency
82.9
83.5
83.8
84.1
83.5
82.5
84.9
82.1
82.1
82.0
81.4
82.1
81.9
81.9
82.1
81.5
82.3
81.5
82.3
82.3
82.9
81.2
79.6
80.9
81.0
79.5
82.5
85.0
86.0
84.0
83.0
87.0
82.5
85.0

-------
                                                                       HOURLY DATA
                     Date
                    (Contd)
                     1-14
U)
o
 I
                     1-1S
                     1-16

                     1-17

                     1-18
Time

2100
2200
2300
2400

0100
0200
0300
0.400
0500
0600
0700
0800
0900
1000
1100
1200
1300
1'KJO
1500
1GUO
1640
                               1330
                               1>400
                               1500
                               1600
                               17002
                                        MW
Inlet SCRUBBER
f*FM 3C
1000 2nd
	 4£_
207.
207.
207.
207.
207.
207.
207.
207.
207.
207.
207.
6.8
7.0
7.0
6.8
6.8
6.8
6.8
6.8
6.8
6.8
6.8
218.1 6.8
218.1 6.8
218.1 6.7
218.1 6.5
218.1 6.6
218.1 6.6
153.6 2.0
218.1 6.8
22M..4 7.0

Stage
pH
7.0
7.0;
7.0
7.0
7.0
6.9
6.8
7.1
7.2
7.1
7.1
7.0
6.9
7.1
7.3
7.2
6.9
7.0
7.3
7.2

S02
£pm
1000
1000
1000
1050
1000
1000
1000
1020
1050
1050
1000
1050
NFl
1300
1280
1260
1270
1250
1280
1280
TMT !"•••
INL
NOX
ppm
400
420
400
390
380
380
380
380
370
380
380
360
NF
360
350
360
360
350
360
360
C.1
C02
Ji_
14.5
I'l.O
1M.O
13.9
13.7
13.9
13.7
13.7
13.9
13.8
13. 8
11.3
NF
13.7
13.6
13.7
14.5
13.0
13.9
13.9

02
_2L
5.5
6.0
6.0
6.0
6.0
5.8
6.0
6.0
6.0
6.0
6.2
NF
NF
6.2
6.1
6.0
6.0
6.5
5.9
6.3

S02
ppm
130
170
180
350
200
180
160
160
150
150
150
100
225
255
260
230
250
270
220
NF
nt |1*T t-*f
OUIL
NOX
ppm
360
360
340
350
350
340
340
340
340
340
340
330
310
310
320
320
330
290
330
NF
C.1
CO2
_2L
13.0
12.0
12.0
12.2
12.0
13.7
12.5
12.7
12.7
12.7
12.5
12.3
12.5
12.2
12.4
12.4
12.7
10.1
12.3
NF

02
JL
7.
7.
7.
7.
7.
7.
7.
7.
7.
7.
7.
7.
7.
7.
7.
7.
7.
8.
7.
NF



1
6
6
4
2
2
5
3
4
4
4
4
4
2
2
2
5
9
5

                                       127
    SCRUBBER DOWN - out of MgO

    SCRUBBER DOWN

    SCRUBBER DOWN

    SCRUBBER DOWN

    SCRUBSF.R On-Mne
126 197.S  5.6   7.5   800
150 188.4  4.2   7.2   940
178 188.4  5.4   7.3   900
 *     *      *     *    *
420   13.3   6.0    I'M)    390   12.6   6.7
450   12.5   6.8    160    425   12.3   6.7
460   13.0   6.5    140    390   11.0   8.4
 *******
                                                                               %  S02
                                                                              Removal
                                                                              Efficiency

                                                                                87.0
                                                                                83.0
                                                                                82.11
                                                                                66.7
                                                                                80.(I
                                                                                82.0
                                                                                84.0
                                                                                84. 3
                                                                                85.7
                                                                                85.7
                                                                                85.0
                                                                                84.8

                                                                                80.4
                                                                                79.7
                                                                                81.7
                                                                                80.3
                                                                                78.4
                                                                                82.8
                                                                                        82.5
                                                                                        83.0
                                                                                        84.4
                               *•  Sample  line  frozen
                               2  Scrubber  shut down 1730,  1.1), fan down

-------
                                                                    HOURLY DATA
                  Date

                  1-19
                  1-20

                  1-21
                  1-22
                  1-23
 I
to
                  1-2M


Time
1130
1200
1300
1'fOO



1MM5
1500
1600
1700
1800
1900
2000
2100
2200
2300
2MOO
0100
0200
0300
OMOO
0500
0000
0700
0800
0900
1000
1100
1200
1300
Inlet
ACFM x
MW 100,0 1
SCRUBBER
177 180.2
175 173.1
*1 NF
SCRUBBER DOWN
SCRUBBER DOWN
SCRUBBER DOWN
SCRUBBER
2nd
A P
Stage
pH
On-Line
3.M
M.M
0



7.5
7.2
*



S02
PPm

10MO
1020
1000



INLET
NOX
PPm

M70
M50
MMO



C02


13.0
12.5
12.5



02
%

6.M
6.8
7.0



S02
ppm

200
210
*



OUTLET
uox
PPm

M50
M20
*



C02
JL

12.5
12.0
*



02
%

7.0
7.0
*



SCRUBBER On-Lim?
181 78.8
178 74.8
170 120.3
178 87.0
178 67.0
178 110.1
181 46.1
177 87.0
171 99.3
172 99.3
179 120.3
176 153.6
176 153.6
168 140.8
168 140.8
108 140.8
170 120.3
175 146.4
176 188.4
17 1| 207.4
178 207.4
175 218.1
176 146.4
1.8
2.0
3.2
2.0
2.0
1.2
1.2
2.M
3.M
M.5
3.6
M.O
3.8
3.8
3.8
3.8
3.8
M.'l
5.7
7.5
8.0
8.5
0
7.7
7.6
6.9
7.1
7.0
6.9
7.1
7.2
7.3
7.2
7.2
7.2
7.1
7.0
7.0
7.0
7.1
7.1
7.3
7.M
7.3
7.3
7.5
1180
1120
1200
1150
1150
1200
1100
1200
1180
1180
1200
1200
1200
1250
1300
1300
1150
1100
870
1050
1020
1080
1070
M50
MMO
M60
MMO
MMO
M30
'100
MMO
M20
M20
MMO
MMO
MMO
MMO
MOO
M20
MOO
M20
•420
M50
M50
M50
MMO
13.1
12.5
13.0
13.5
13.5
1M.O
13.11
13.8
13.0
13.5
13.5
13.5
13.5
13.5
1U.5
13.5
13.5
13.3
1M.1
1M.M
1M.3
1M.2
13.7
6.6
7.2
6.M
5.6
6.5
6.2
7.1
6.M
6.6
6.2
6.M
6.2
6.M
6.M
M.8
6.M

O.M
6.2
6.8
6.8
6.5
7.0
110
300
280
320
300
290
290
270
250
290
2MO
2MO
. 2MO
200
2MO
250
270
200
120
120
115
120
255
370
M20
MMO
MOO
MOO
380
380
3 MO
360
380
380
380
380
390
380
360
3 MO
370
360
M.O
M10
M20
260
10.8
12.0
11.8
11.8
13.0
13.0
12.5
11.5
11.5
U.5
11.5
11.5
11.5
12.5
12.0
12.5
12.0
12.2
12.9
12.5
13.2
13.6
9.1
8.6
8.0
7.M
7.14
7.2
8.0
8.0
9.0
8.0
8.0
8.M
8.2
8.M
7.8
8.0
8.2
8.M
7.8
7.8
8.2
8.2
7.8
10.0
                                                                                                                 % S02
                                                                                                                Removal
                                                                                                               Efficiency
                                                                                                                  80.8
                                                                                                                  79.M
90.7
73.2
76.7
72.2
73.9
75.8
73.6
77.5
78.8
75.M

80.0
80.0
80.0
8M.O
81.5
80.8
76.5
81.8
                                                                                                                  86
                                                                                                                  88
                                                                                                                  88
                                                                                                                  88
                                                                                                                  76.2
                              Scnibbor  down at 1MOO, 1st stage overflow

-------
 I
w
CO
CO
SCRUBBER

Date
1-24
(Contcl)









1-25















Time
1400
1500
J600
1700
1800
1900
2000
2100
2200
2300
2UOO
0100
0200
0300
OUOO
0500
0600
0700
0800
0900
1000
1100
1200
1300
I'lOO
1500-2400
Inlet
ACFtl x
MW 1000
172 135,7
175 197.6
176 242.2
176 255.0
J82 266.2
176 279.6
1R3 266.2
178 207.4
178 218.1
17M 218.1
174 218.1
175 218.1
178 2^8.4
179 228.4
172 242.2
141 228.4
140 255.0
138 255.0
158 218.1
177 228.4
176 NF
175 218.1
177 197.6
175 188.4
177 197;. 6
2nd Stage
.AP
1.0
4.5
3.4
3.2
3.0
3.4
3.0
8.0
8.0
8.0
7.5
7.6
9.0
9.0
9.5
9.5
9.5
9.5
6.5
8.8
9.0
9.0
8.8
8.8
8.8
SCRUBBER DOWN
pH
7.3
7.2
7.5
7.2
8.3
7.8
7.8
7.3
6.9
7.1
7.1
7.1
7.2
7.1
7.0
7.1
7.1
7.1
7.2
7.2
7.1
7.0
7.1
7.1
7.1
S02
PPii
1060
1050
1050
1000
970
980
940
920
920
950
950
900
900
900
900
900
900
1000
980
1050
1000
1000
1000
1010
1020
- Leaks In
HOURLY DATA
INLET
MOX CO2
ppm
415
440
440
420
420
430
420
420
420
430
410
410
410
400
400
410
440
440
420
430
420
420
400
400
410
•%
13.5
13.8
14.5
16.0
13.5
14.5
14.5
14.0
13.0
13.5
12.5
12.2
12.0
13.5
13.5
11.5
14.0
13.5
12.7
15.6
13.5
13.5
13,7
14.5
13.0
02
JL
6.8
6.7
6.5
6.0
7.0
6.4
7.0
6.6
6.8
6.4
6.6
6.4
7.0
6.4
6.6
6.4
6.4
6.4
6.9
6.2
6.1
6.2
6.3
6.4
6.2
S02
ppm
300
310
310
680
700
6RO
690
130
130
140
120
120
120
100
100
100
110
140
130
120
115
120
120
120
120
OUTLET
NOX C02
ppm
370
420
420
410
420
420
410
360
360
360
360
360
360
360
360
380
410
400
370
380
380
370
360
370
370
%
12. 3
13.7
13.5
15.5
13.5
14.0
14.0
11.5
12.0
11.5
11.5
11.5
11.2
12.0
12.0
14.0
13.0
12.5
11.3
11.2
11.7
11.5
12.6
12.5
11.9
02
_2L
8.8
7.2
7.0
8.0
7.0
7.0
7.0
8.5
8.0
8.2
8.0
8.0
8.0
8.0
7.8
6.8
7.8
8.0
7.6
8.1
7.2
7.6
7.8
7.7
7.6
% S02
Removal
Efficiency
71.7
7(1.5
70.5
32.0
27.8
30.6
26.0
85.9
85.9
85.3
87.il
86.7
86.7
88.9
88.9
88.9
87. R
86.0
86.7
88.6
88.5
88.0
88.0
88.1
88.2
1st stage
                  1-26

                  1-27   0100-0500
                            06001
                            0700
    SCRUBBER DOWN

    SCRUBBER DOWN
116   NF     .7    7.4
163   NF    1.8    7.4
1000
1000
400
440
13.8
12.0
7.0
7.2
280
280
310
380
12.5
11.5
8.0
8.6
72.0
72.0
                            1 Start up 0525

-------
                                                                     HOURLY DATA
 I
CD
to
U)
 I


Date
1-27
(contd)







1-28
1-29
1-30 to
8-11











8-12


Time
0800
09001
1000
1JOO
1200
1300
moo
15002
1000-2400


8/10
0100-1300
1M3&3
15004
1000
1700
1800
1900
2000
2100
2200
2300
2UOO
0100
Inlet SCRUBBER
ACFM x 2nd Stage
MW 1000 4P pH
176 nF 0.2 7.5
162 309.2 13.0 7.5
116 255.0 10.8 7.<4
138 242.2 10.2 7.2
17'l 207.4 8.0 7.2
175 207.4 7.8 7.3
17M 228.4 8.0 7.1
173 108.4 2.2 7.2
SCRUBBER DOWN
SCRUBBER DOWN
SCRUBBER DOWN
INLET •
S02
ppm
9UO
900
910
9"4<)
1020
1020
1020
1010

- Test
- Test
Boiler and Scrubber

185 87.0 1.7 *3
185 100.2 1-8 *
182 180.2 2-7 *
185 207.4 3.0 *
182 218.1 2.6 7.7
182 218.1 3.3 *
183 218.1 3-t 7.3
18'« 218.1 3.3 *
183 218.1 3.'» 7.1
183 218.1 3.2 *
183 218.1 3.2 7.0
18'l 218.1 3.2 *

10
660
700
700
670
680
680
680
700
6'IO
600
600
NOX
C02
ppm %
mo
'110
•400
'•60
510
520
520
U80

crew
crew
13.0
13.5
13.5
14.1
13.3
13.2
13.3
1«4.S

parked up
left site-
02
_2L
7.0
7.5
6.9
6.2
7.0
8.5
6.7
7.0

S02
ppin
240
63
80
105
130
125
125
160

OUTLET
NOX
ppm
380
UOO
390
M60
'150
M50
U50
<420

C02
JL
ii.i
12.2
12.9
13.3
12.0
11.8
11.5
12.7

02
_*_
8.5
8.6
7.8
6.7
8.5
8.5
6.7
7.0

% S02
Removal
Efficiency
73. 3
93.0
91.2
88. R
87.3
87.7
87.7
8U.2

equipment

down for maintenance

NF
Nr
NF
NT
NF
NF
NF
NF
NF
NF
NF
NF

.5
12.0
12.5
12.3
12.5
12.5
12.5
12. S
13.0
13. 0
13.0
12.5

*
*
6.0
6.2
6.2
6.1
6.0
6.0
6.0
6.1
6.0
6.0





and repairs

590
130
130
130
110
110
itro
110
110
100
100
90

NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF

11.5
12.M
12.2
10.0
10.5
10.5
10.5
10.5
10.5
10.5
10.5
10.5

*
*
6.8
8.8
8.6
8.U
8.5
8.6
8.5
8.6
8.7
8.8

-
80.3
81. H
81.14
83.6
83.8
85.3
83.8
814.3
BM.M
83.3
85.0
                            1  High c;as Flow 0815
                            2  Scrubber down 15<40
                            3  Trailer readings suspect until 1000, 8/12
                            "  Scrubber start up

-------
                                                                  HOURLY DATA
               Date


               8-J2
               (Con td)
03
W
**
 I
               8/13


Tnloh
ACFfi x
Time
0200
0300
0400
0500
OGOO
07 (JO1
08002
0900
1000
1100
1200
1300
1400
1500
1600
1700
1800
1900
2000
2100
2200
2300
2400
0100
0200
0300
0400
0500
OGOO
0700
MW
162
I'll
151
177
ISO
ISO
183
184
186
187
185
185
185
184
185
184
184
183
185
183
184
181
184
179
185
181
180
155
1G4
186
1000
242.2
242.2
218.1
228.4
242.2
228.4
188.4
197.6
197 < 6
197.6
197.6
197.6
197.6
197.6
188.4
197.6
197.6
197.6
197.6
197.6
207.4
207.4
207.4
197.6
197.6
197.6
218.1
210.1
207.4
207.4
RrnimRER INLET
2nd Stage
A P
3.7
3.7
3.7
3.3
3.3
3.3
4.0
2.9
2.5
2.9
3.0
3.0
3.0
3.0
3.0
3.0
3.0
3.0
3.0
3.0
3.0
3.0
3.2
2.8
2.8
2.8
3.5
3.6
3.2
3.2
pH
7.0
*
7.0
*
7.0
*
0.8
*
6.8
*
7.1
*
7.0
*
7.1
*
7.1
*
7.1
*
6.8
*
7.0
*
7.0
*
7.0
*
7.1
*
S02
ppm
600
590
550
GOO
GOO
NF
780
NF
1020
NF
1080
NF
10RO
NF
1140
NF
1140
NF
1140
NF
1140
NF
1140
NT
1140
NF
1200
NF
1200
NF
NOX
ppm
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
C02

12.5
13.0
13.0
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
02
*
5.9
G.O
5.6
5.8
5.8
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
SOj
ppm
90
90
90
80
90
NF
294
NF
300
NF
300
NF
300
NF
300
NF
300
NF
300
NF
300
NF
300
NF
262
NF
300
NF
300
NF
GliTLiM
NOX
ppm
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
C02
_2L
in. 5
10.5
11.0
NF
NF
NF
NF
NF
NF
.NF
NF
NF
NF
NF
NF
NT
NF
NT
NF
NF
NF
NF
NF
NT
NF
NF
NF
NF
NF
NF
02
JL
8.6
8.6
8.3
8.4
8.3
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
*j s
-------
                                                                     HOURLY PATA
U)
Ul
I



Inlet
ACFH x
Date
8/13
(Contd)















8/14













Time
0800
0900
1000
1100
1200
1300
1400
1500
1000
1700
1800
1900
2000
2100
2200
2300
2400
oiooi
0200
0300
0400
0500
0600
0700
0800
0900
1000
1100
1200
1300
1400
MW
184
184
182
183
180
183
182
181
183
184
185
184
187
184
184
184
188
183
186
170
150
151
150
178
183
186
184
181
181
178
178
1000
218.1
218.1
218.1
218.1
218.1
210.1
207.4
207.4
207.4
207.4
218.1
213.1
207.4
207.4
207.4
207.4
120.3
120.3
135.7
66.6
66.6
66.6
66.6
66.6
82.9
87.0
82.9
82.9
82.9
82.9
02.9
SCRUBBER
2nd Stage
j&P
3.3
3.3
3.3
3.0
3.6
3.0
3.0
3.8
3.8
3.8
3.8
3.8
3.8
3.8
3.8
3.8
2.8
1.4
1.4
2.0
0.4
0.4
0.4
0.3
0.8
0.8
0.8
0.8
0.8
0.8
0.8
pH
7.0
*
7.0
*
7.1
*
7.0
*
7.1
*
7.1
*
7.1
*
0.9
*
7.1
*
7.2
*
7.4
*
7.3
*
7.1
*
7.1
*
7.1
*
7.1
S02
ppm
1140
NF
1140
NF
1080
NF
1.170
NF
1200
NF
1260
NF
1260
NF
1260
NF
1200
NT
1260
NF
1080
NF
1080
NF
1080
NF
1080
NF
1020
NF
1020
INLET
NOX
PPm
NF
NF
NF
NF
NF
NF
NF
NF
NF
NT
NT
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
C02
%
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NT
NF
NF
NF
NF
02
JL
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
S02
ppm
294
NF
294
NF
2'40
NF
270
NF
300
NF
300
NF
300
NF
300
NF
360
NF
360
NF
180
NF
180
NF
240
NF
240
NF
240
NF
240
OUTLET
NOX
ppm
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NT
NF
NF
NF
NF
C02
JL
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NT
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NT
NF
NF
NF
NF
02
JL
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
% S02
Removal
Efficiency
74.2
_
74.2
_
77.8
-
76.9
.
75.0
_
76.2
_
76.2
_
76.2
_
71.4
_.
71.4
_
83.3
_
83.8
_
77.8
_
77.8
_
76.5
-
76.5
                              DuPont SOj readings

-------
                                                                  HOURLY DATA
 I
CO
u>
Inlet SCRUBBER

Date
8-14
(Contd)








8-15



8-16
8-17
8-18
8-19
8-20
8-21
8-22





Time
1SOO
1000
1700
1800
1900
2000
2100
2200
2300
2400
oiooi
02002
03003
0400-2400






0100-1400
14301*
15003
1GOO
17 00&
ACFM x «?nd
MW j&aa. 4?
179 32.9 0.8
179 32.9 0.8
177 105.0 1.3
177 110.1 1.3
178 140.8 2.3
179 140.8 2.4
183 165.9 3.0
178 165.9 3.0
178 130.2 3.5
179 180.2 3.5
181 188.4 3.6
178 188.4 3.8
178 207.4 4.1
SCRUBBER DOWN
SCRUBBER DOWN
SCRUBBER DOWN
SCRUBBER DOWN
SCRUBBER DOWN
SCRUBBER DOWN
SCRUBBER DOWN
SCRUBBER DOWN
176 * 1.5
175 153.6 2.0
177 165.9 2.0
179 173.1 2.0
Stage SO2
pH
*
7.1
*
7.0
*
6.9
*
7.0
*
7.1
*
7.2
*








*
*
7.4
*
ppm
NT
900
NF
900
NF
1020
NF
1020
NF
1020
NF
1080
NF








NF
1150
1200
1190
INLET
•NOx
ppm
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF








NF
NF
NF
NF
C02
_*_
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF








NF
13.0
13.5
14.5

02
_2L
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF








NF
6.0
6.0
6.1

S02
ppm
NF
240
NF
240
NF
240
NF
240
NF
240
NF
240
NF








NF
370
350
340
OUTLET
NOX —
ppm
NF
NF
NF
NF
NT
NF
NF
NF
NF
NF
NF
NF
NF








NF
NT
NF
NF
CO2
_2L
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF








NF
13.0
12.5
12.7

02
_2L
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF








NF
7.8
7.3
7.2
% S02
Removal
Efficiency

75.0
-
75.0
-
76.5
-
76.5
-
76.5
_
77.8
-








_
67.8
70.8
71.4
                         1 DuPont SO2 readings
                         ' Dryer plugged
                         3 Scrubber down 0400 - dryer pluggrd
                         '* Scrubber start up
                         * Trailer on line
                         ^ Velocity increase 1630

-------
                                                                     HOURLY DATA
                   Date

                  8-22
                   (Contd)
                  8-23
W
CO


Inlet
ACFM x
Time
1800
1900
2000
2100
2200
2300
2400
0100
0200
0300
0400
0500
06001
0700
0800
0900
1000
1100
1200
1300
1400
1500
16002
1700
1800
1900
2000
21003
2200
2300
2400
MW
184
180
177
181
178
176
178
184
181
170
138
117
116
115
116
125
171
177
181
176
180
174
171
170
182
181
174
180
178
174
158
1UUO
207.4
207.4
207.4
207.4 .
197.6
197.6
197.6
197.6-
180.4
218.1
228.4
228.4
228.4
228.4
223.4
218.1
207.4
207.4
207.4
197.6
207.4
207.4
207.4
207.4
197.4
207.4
207.4-
207.4
146.4
146.4
120.3
SCRUBBER
2nd
>4 P
3.2
3.4
3.4
3.4
3.4
3. 4
3.4
3.4
4.2
4.2
4.2
4.2
4.2
4.2
4.2
4.2
3.7
3.7
3.7
3.7
3.7
3.7
3.5
3.2
3.2
3.2
3.2
3.2
1.5
1.0
1.0
Stage
pH
7.3
*
7.2

7.2
*
7.0
*
7.0
*
6.9
*
6.9
*
6.9
*
7.1
*
7.1
*
6.9
*
6.9
*
7.0
*
7.0
*
7.0
*
*
S02
ppm
1150
1090
1100
1095
1100
1000
1000
1100
1040
1025
1090
1075
1020
NF
1140
NF
1200
NF
1200
NF
1380
NF
1380
NF
1440
NF
1500
NF
1080
NF
NF
INLET
NOX
ppm
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
C02
%
13.5
13.7
12.5
13^0
12.5
13.4
13.4
13.3
13.2
•13.3
13.0
13.1
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
02
%
5.6
6.2
6.2
6.2
6.5
6.4 •
6.4
6.5
6.7
6.5
6.7
6.9
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
S02
ppm
300
290
300
300
295
270
280
290
300
270
250
250
180
NF
300
NF
300
NF
300
NF
420
NF
390
420
400
400
410
400
500
470
500
OUTLET
NQX
Ppm
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
C02
%
12.5
12.0
12.3
12.0
11.9
12.5
12.6
12.6
12. .6
12.7
12.5
12.5
NF
NF
NF
NF
NF '
NF
NF
NF
NF
NF
12.0
12.6
12.6
12.8
12.8
12.7
12.3
12.4
12.3
02
%
6.6
7.2
7.2
7.3
7.4
7.4
7.2
7.3
7.6
7.4
7.5
7.7
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
7.4
7.0
6.8
6.8
6.6
6.7
7.8
7.0
7.6
% S02
Removal
Efficiency
73.9
73.4
72.7
72.6
73.2
73.0
72.0
73.6
71.2
73.7
77.1
76.7
82.4
-
73.7
-
75.0
-
75.0
-
69.6
_
71.7
-
72.2
-
72.7
-
53.7
' -
-
                            •*• DuPont SOj readings, conditioners malfunctioned
                            2 Outlet mode of trailer on-line
                            3 Centrifuge Clog

-------
                                                                   HOURLY DATA
tfl
U)
00
 I
Date Time
ACFM x
MW 1000
8-24 SCRUBBER DOWN -
8-25 • SCRUBBER DOWN -
1330
14001
15002
1600
1700
1800
1900
2000
2100
2200^
2300
2400
8-26 0100
0200
0300
04001*
0500
0600
0700
0800
0900
1000
1100
1200
1300
1400
184
175
178
182
180
176
177
175
182
173
171
180
177
179
182
176
183
180
176
177
176
178
180
184
185
185

173.1
173.1
180.2
180.2
180.2
173.1
180.2
188.4
188.4
188.4
188.4
188.4
138.4
.188.4
197.6
197.6
197.6
125.4
125.4
120.3
120.3
146.4
146.4
173.1
197.6
2nd
Stage S02
pH ppm
0305
0100-1300
0.0
1.8
3.2
3.2
3.2
3.2
3.2
3.2
3.2
3.2
3.2
3.2
3.2
3.2
3.2
3.2
0.7
3.4
0.8
0.9
0.9
0.8
1.6
1.6
2.8
3.6

7.3
*
7.3
*
7.3
*
7.3
*
7.0
*
7.0
*
6.9
*
6.9
*
6.9
*
7.2
*
7.1
-*
7.1
*
6.8


1080
NF
1140
NF
1140
NF
1140
NF
1250
1325
1325
1275
1200
1175
1300
1200
1300
1350
1300
1325
1300
1225
1200
1150
1050
NOX C02
ppm • %


NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NT
NF


NF
NF
NF
NF
NF
NF
• NF
NF
13.0
13.7
12.8
12.6
12.6
12.5
12.5
12.5
12.5
13.0
13.0
13.5
12.9
1U.O
14. 4
14.6
14.5
02
-3L


NF
NF
NF
NF
NF
NF
NF
NF
5.8
5.8
5.8
5.8
5.3
5.8
6.1
6.6
5.9
6.5
6.6
6;6
6.8
6.2
6.3
6.0
5.9
S02
PPm


360
NF '
310
320
340
310
310
340
350
375
380
380
350
360
390
400
400
400
425
480
425
400
400
300
290
NOX
PPffl


NF
NF
NF
; NF
NF
NF
NF
NF
NF
NF
NF
NF
KF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
NF
C02


NF
NF
13.0
12.9
11.5
12.5
12.5
12.7
12.5
13.0
11.6
11.6
11.5
11.5
12.0
10.5
11.8
11.0
12.0
12.2
11.5
12.7
13.5
13.3
14.0
02


NF
NF
6.7
7.4
7.4
7.4
7.0
C.8
7.0
6.8
6.9
6.9
7.1
7.0
7.0
9.0
7.1
7.0
8.6
8.4
8.7
8.0
7.2
7.2
6.7
Removal
Efficiency


66.7
_
72.8
-
70.2
_
72.8
_
72.0
71.7
71.3
70.2
70.8
69.4
70.0
66.7
69.2
70.4
07.3
63. B
67.3
67.3
67.7
73.9
72.4
                          1 DuPont SOg .inlet readings
                          2 Scrubber start up
                          3 Trailer On-line
                            Velocity change

-------
                                                                         HOURLY DATA
OJ
VD
I
Inlet SCRUBBER

Date
8-26
(contd)








8-27
















Time
1500
1600
1700
18001
1900
2000
2100
2200
2300
2400
0100
0200
0300
0400
0500
0600
0700
0800
0900
1000
1100
1200
1300
14002
1500
1530-2400

ACFI1 x 
-------
-B40-

-------
      APPENDIX C
DAILY OPERATING LOGS
          -Cl-

-------
-C2-

-------
NOVEMBER 1974
      -C3-

-------
1974

Nov. 1 - The scrubber was not in operation.  The hub for the "B"
         MgO pump was not available; operators settled for reboring
         the old hub and reassembled the pump.  A new 3HP motor
         was installed on dryer conveyor.  Some attention and
         effort was placed on reducing the spillage when loading
         MgS03.

Nov. 2 - The centrifuge cover was installed as was the vibrator
         on the MgSC>3 silo.  Work was completed on the pipe
         line, and the 14 inch discharge line at the "B" recycle
         pump  (first stage) was finished.  Installation of a
         pump coupling on the "B" MgO slurry pump was accomplished
         and a truck load of MgO was received.

Nov. 3 - Sunday

Nov. 4 - Welding contractor began repairing various pipes.  The
         man-way on the first stage was opened.

Nov. 5 •- Inspected first stage inner cone.  One break in the
         lining in compression ring of inner skirt under the
         modules was noted but no repairs were initiated.  The
         rod below the hanger was fine as was the plumb bob.
         The vortex breaker showed signs of erosion or etching.
         The hangers supporting the first stage cone were
         acceptable.

Nov. 6 - The first stage man-ways were closed.  An outboard
         bearing on the top of the bucket elevator was worn
         out.  Repairs were made on leaHs in the steam line
         and on the top of the scrubber.  All bearings were
         lubricated and the oil levels checked.  The plumb bob
         was operated as a check.

Nov. 7 - Work was done on cutting out and cleaning the "A" MgO
         line.  A leak was fixed in the sump pump discharge line.
         The car of MgO was unloaded.  Completed work on Suction/
         Discharge headers except for "patches" or overlay
         pieces, which still needed welding.

Nov. 8 - Installed bearing on top of the bucket elevator.  Work
         on the MgO pumps and lines has been completed; pump
         performance will be tested.  The fir^t stage was filled
         and leak tested.

Nov. 9 - The centrifuge was started for pre-run time.  The MgO
         storage tank was heated.  The thickeners were refilled.
         The weigh belts were recalibrated and zeroed.  All
         solids handling equipment was test run.  Water was
         introduced into the second stage-  At 1600 hours the
         "B" MgO pump stopped.  An electrician was called to
         install a larger heater in the switch.  By 2000 hours


                              -C4-

-------
          the pump was back in service.  The "A" MgO line was
          well flushed with hot water.  The level of MgO was
          lowered to 20% and the first batch was prepared at
          2100 hours.  The man-ways on the gas ducts were closed.

Nov. 10 - At 0140 hours the fan was started but it tripped out
          because the damper did not open.  At 0145 the fan was
          started again and gas went through the scrubber.  At
          0300 hours the flow was raised to 148,000 ACFM.  The
          pH was erratic due to the malfunctioning of the meter
          in the scrubber control room.  At 0800 hours the
          solids handling equipment was put on line.  The MgO
          slurry in the tank turned to putty at 0930, and the
          load was reduced to 94,000 ACFM.  A new batch of MgO
          was made and at 1245 hours the load was brought to
          118,000 ACFM.  Since the pH was not held constant during
          this period of operation, many changes in flow were
          experienced.  At 1645 the steam control valve on the
          MgO tank failed to control the temperature, the steam
          to the tank was then put on manual control.  At 2300
          hours, a hole was discovered in the mother liquor
          return line on the second stage of the scrubber.

          The continuous monitoring trailer experienced some
          problems after start up.  Probe filters had to be
          altered as they were restricting flow.  Temperatures
          in the conditioning system had to be changed due to
          moisture reaching the analyzers.  S02 readings from
          0220 to 0745, 02 readings from 2045 through midnight
          and CC>2 readings all day may be incorrect because of
          these problems.

Nov. 11 - At 0245 hours the stack gas was routed out of the
          scrubber, so repairs could be made.  The following
          problems were noted at this time:  a broken electrode
          and a leak in the pH meter system, a plugged MgO line
          to the absorber, and the recycle slurry line from the
          absorber to the centrifuge was parted at the discharge
          header.  The steam controller on the steam line to the
          MgO tank was found to be operating properly, but it
          appeared the check was sticking.  A mechanic was not
          available today from either Pepco or Hurley.

Nov. 12 - The MgO tank was drained and flushed in an attempt
          to find the restriction in the line to "B" pump.  The
          instrumentation department worked on the temperature
          monitor and steam control check valves.  Changes were
          made in the continuous monitoring system so the SO-
          unit could automatically change scales for inlet/
          outlet modes.

Nov. 13 - Four mechanics from Hurley reported for work in the
          morning.  The thermocouple for temperature monitoring
          in the circulation line was placed in the vertical
                               -C5-

-------
          position for more effective readings.  Gas was routed
          into the scrubber at 2010 hours.  The pH meter was still
          not functioning correctly but the steam line to the MgO
          tank was working properly.  The loading was increased
          to 148,000 ACFM at 2130.

          A probe blow-back system for the continuous monitoring
          trailer was installed and made operative.  This should
          reduce flow problems caused by probe plugging.  The
          sampling site for mother liquor samples was changed in
          order to take a more representative sample.  York
          Research personnel were asked to take pH readings
          every 15 minutes as the scrubber plant pH meter was
          not working properly.

Nov. 14 - The scrubber operated all day.  The batch of MgO appears
          to have had low reactivity.  Research is needed to
          evaluate the quality of the MgO effect on slurry tank
          temperature and its reaction with mother liquor to
          determine why the slurry jelled again as it did on
          Nov. 10th.  The centrifuge drop-out hopper plugged up
          and had to be cleaned out.  The "B" thickener dump
          valve fully opened causing the dilution tank to over-
          flow.  Electricians were called to make repairs to the
          MgO Belt indicator, heat tape, rake lowering mechanism
          and MgSC>3 weigher motor.  The steam line valve to the
          MgO tank was shut off to observe the effect.

          The continuous monitoring system was operational but
          some problems developed with leakage and outlet probe
          blockage.  These were corrected during the day.  The
          SO? readings from 0530 to 0830, C>2 until 0830 hours
          and C02 readings may have been incorrect,,

          York personnel were performing pH tests every half hour
          in order to check the accuracy of the scrubber plant pH
          meter.

Nov. 15 - The scrubber was operated all day today.  Early in the
          day the flow had to be reduced to 110,000 ACFM from
          160,000 ACFM due to foreign material plugging the weigh
          feeder belt.  The flow was brought back up when the
          problem was corrected.

          The centrifuge cover was removed and the hopper was
          cleaned out.  There was no spout extension for use
          when loading MgSCK, as was requested on Nov. 1.  There-
          fore, approximately 1.5 tons of MgSOo were spilled.
          When stripping the crystals which had accumulated in
          the absorber while the centrifuge was being repaired,
          it was found the maximum flow to the centrifuge was
          55 gpm.  This may be a limiting factor in the amount of
          gas sent to the absorber.  The pH meter had to be
          repaired and was working properly by 1600 hours.  The


                               -C6-

-------
          north thickener was put into operation as a leak
          developed in the cone of the south thickener.

          Holland Glenn requested York chemists to take two
          centrifuge cake samples per day and prepared them
          for shipping to Rumsford, Rhode Island.  (Essex
          Regenerating Plant)

          The C02 readings for the entire day are probably in-
          correct due to an electrical problem within the monitor.

Nov. 16 - York chemists were asked to verify the buffer solution
          used for the pH meters.  Both meters  (bench and con-
          tinuous) were found to be about 0.3 pH units high.
          The MgSC>3 conveyor at the top of the silo tripped and
          the centrifuge was diverted.  The MgSOo weigh belt
          broke and was placed on by-pass.  The bucket elevators
          and centrifuge product screw malfunctioned in late
          afternoon and had to be reset.  The bucket elevator
          kept malfunctioning during the evening and had to be
          dug out and reset numerous times.  At about 1800 hours
          the flow was reduced due to a low pH and the problems
          with the bucket elevator.  A 6 inch pinch valve to the
          tangential spray ruptured at 1930 hours.  Gas was
          taken out of scrubber at 2135 hours.  The second stage
          was operated until 0400 Nov. 17 to strip out the
          solids.

          The continuous monitoring trailer was operating until
         '1000 hours when it was shut down to replace the outlet
          probe with one of better design.  The sample lines
          also had to be flushed out.  Monitoring continued at
          1900 hours.  The C02 readings are probably inaccurate.

Nov. 17 - The scrubber was not in service today.  The equipment
          downstream of the scrubber was washed out.  The screw
          conveyor from the dryer to the bucket elevator was
          inspected.  The gear box needs to be inspected more
          carefully as it is very noisy.  The south thickener
          finished draining during the day.

Nov. 18 - The scrubber was not in service today.  Three Hurley
          mechanics were in working on a first stage line.  It
          was found the key in the drive sheave of the dryer
          screw conveyor was loose and worn, and it was repaired.
          PEPCO operators removed the bolts from the centrifuge
          cover and the second stage discharge header was found
          to be drained.

Nov. 19 - The scrubber was not in service at the start of the day.
          The agitator on "A" dilution tank was hooked up elect-
          rically and filled with oil.  It was then ready for
          service.  The mechanical seal on "B" pump was leaking
          badly when it was started.  The liner was removed and
          replaced in the centrifuge divert valve.  Eleven bolts


                              -C7-

-------
          in the "B" thickener were found to be nearly decomposed
          and were replaced.  Gas went to the scrubber at 1740
          hours.  The centrifuge cover was still leaking.

          Continuous monitoring trailer was operating well after
          the first two hours of operation.  A bad solenoid
          valve caused false readings until approximately 2030
          hours.  The CC>2 readings are probably inaccurate.

Nov. 2C - The scrubber operated all day.  At the start of the
          day, the flow had to be reduced to remove some debris
          from the MgO belt.  By 0100 hours the load had been
          increased to 82% of design.  The impeller was removed
          from "A" recycle pump and Chemico personnel requested
          PEPCO to order a back-up one.  The bearing on the
          inside of Dryer #2 conveyor to the silo had come apart.
          This was what probably caused the conveyor to trip on
          Nov. 16.  A new leak developed in the centrifuge cover
          during the day.

          The continuous monitoring trailer was semi-operational,
          with the S02 unit output very low and the CC>2 unit
          down  (C02 readings were taken by EPA Method 3).

          The chemical trailer operation was normal.  Some special
          analyses were performed on the sump discharge, the
          process water and the second stage bleed.  Also some
          changes were made in analytical procedures due to the
          detection of interferences in some of the samples.

Nov. 21 - The scrubber operated most of the day.  At 0110 hours
          the bucket elevator tripped.  The load reduced by about
          45,000 ACFM at 0130 hours to reduce the build-up of
          crystals.  The temperatures associated with the dryer
          did not appear correct but this may have been due to one
          of the thermocouples having been located near an air
          leak from outside the dryer.  The front rappers fell
          off the dryer in the morning, causing the thermocouples
          to the fire box to be ripped out.  The centrifuge
          hopper had to be washed out and an attempt was made
          to weld the holes in the centrifuge cover.  At 1520
          hours the flow was reduced to 187,000 ACFM to reduce
          crystal formation.  At 2000 the belts on the dryer ID
          fan burned off, and the gas was removed from the scrubber,
          A mechanic was called out to replace the belts.

          The continuous monitoring trailer was semi-operational.
          The S02 and CO2 units were repaired during the day.

          Meetings were held by York, PEPCO and Chemico repre-
          sentatives.

Nov. 22 - The scrubber did not operate today.  An electrician
          was called in at 0030 hours to check the fan.  The
          housing was half filled with water; it was drained,


                              -C8-

-------
          but it still would not perform at the proper speed.
          The duct and dryer man-way covers were removed and the
          #2 screw conveyer was inspected.  The mechanics re-
          moved the dryer fan pulley for replacement.  The
          centrifuge cover was welded again today.  Two trucks
          each removed a load of MgSC>3.  An unsuccessful attempt
          was made at cleaning the second stage overflow line.

Nov. 23 - The scrubber did not operate.  The work on the rappers
          and on the dryer ID fan was completed.

Nov. 24 - The .scrubber operated for part of the time.  At 0240
          hours, gas entered the scrubber.  At 0830 hours,
          the gas was taken out of the scrubber as the sheave
          bushing in the dryer gear box was the wrong size.
          The sheave was replaced and the scrubber was started
          at 1445 hours at 153,600 AFCM.  By 1900 hours the flow
          was up to 218,100 ACFM.

Nov. 25 - The scrubber operated all day.  The flow was cut back
          to 82,900 ACFM.  The bucket elevator and screw conveyor
          had to be cleaned out.  By 0400 hours the load had
          been increased to 91,100 ACFM.  At 0945 hours the flow
          stabilized at 175,000 ACFM.

          The continuous monitoring trailer operated well except
          for some outlet flow problems which were corrected as
          soon as they occurred.

Nov. 26 - The scrubber operated all day with a flow of 165,000
          ACFM.  Repair work began on the south thickener valves.
          During the day the cover and hopper from the centrifuge
          had to be washed out.  A leak developed in a 6 inch
          water recycle line on the first stage and it was
          sealed with a rubber lined clamp-on band.

          The continuous monitoring trailer had some flow
          problems.  These were attributed to icing in an un-
          heated part of the sampling line.  Heating tape was
          installed to correct the problem.

Nov. 27 - The scrubber operated all day.  The level control on
          the first stage and MgO tank were not working properly
          and had to be repaired.  The maintenance department
          finished installing the valve on the south thickener.
          Variations in pH during the day have been attributed
          to coal feeder problems in the plant, which affect the
          inlet SC>2 concentrations.

          The continuous monitoring trailer was not operational
          during most of the day because of a pump failure.
          Several unsuccessful attempts were made to repair the
          pump.  Before the pump failure, an SO- comparison test
          had been made on the duct, trailer ana analyzer.  The
          readings differed by 6%.


                               -C9-

-------
Nov. 28 - The scrubber operated all day but with some problems.
          A leak developed in the first stage ball nozzle dis-
          tribution header and had to be patched.  The drain
          nipple on the bottom of the sump pump discharge line
          also started to leak.  The feed was diverted because
          the dryer drum had become over-loaded.  This was re-
          flected in the very wet consistency of the centrifuge
          product.  The centrifuge case started leaking worse
          than it had been and the continuous pH meter was not
          operating properly.

          One York chemist was on hand during the day shift
          during this holiday period.

Nov. 29 - The scrubber operated all day.  A leak developed in the
          line from the first stage to the distribution box.  The
          load was reduced in order to maintain the pH while the
          boiler output was reduced.  Patch clamps were installed
          in the 6 inch bleed line, recycle line, and on the
          discharge header of the first stage.  The dryer became
          overloaded again and the centrifuge feed had to be
          diverted to allow the dryer to clear out.  At 1745
          hours the load was increased.  The south thickener was
          filled with water and placed on standby.

          The sampling pump on the continuous monitoring trailer
          was replaced during the day and the trailer was made
          operational.

Nov. 30 - The scrubber operated all day.  Some problems were en-
          countered maintaining pH due to boiler fluctuations.
          The centrifuge hopper had to be washed out during the
          day.  The load was increased to 228,400 ACFM at 1020
          hours.

          The continuous monitoring trailer was operational but
          some flow problems developed.
                               -CIO-

-------
DECEMBER, 1974
       -Cll-

-------
Dec.  1 - The scrubber operated most of the day but had many
         problems.  The torus sprays in the southwest corner
         gave way.  At 0800 hours flow was stopped to the
         torus sprays but the Chemico operator was unable to
         remove the flange bolts to insert the blind.  The
         flow was restored to the sprays but at a reduced rate.
         The 6 inch scrubber bleed to thickener line developed
         another leak but no pipe clamps were available to
         patch it.  The gas was taken from the scrubber at 2200
         hours because the first stage level could not be con-
         trolled.

         The continuous monitoring trailer operated part of the
         day.  The down time was attributed to flow and electrical
         problems.  These were corrected by 0900 hours.

Dec.  2 - The scrubber did not operate today.

Dec.  3 - The scrubber did not operate.  Blanks were installed
         in two lines at the top of the scrubber.  While cleaning
         the pre-mix tank, the laborers dropped a bar into the
         down-comer and it had to be drained to remove the bar.
         The 1 inch mother liquor line to the pre-mix tank broke
         and had to be replaced.  A rubber insert was to be used
         on the 6 inch line to the thickener until a new section
         of line was ready  (approx. Dec. 9).  A first stage
         elbow section of line was removed from the top of the
         scrubber; a replacement was made and will be ready for
         rubber lining tomorrow.

         York chemists performed special analyses while the con-
         tinuous monitoring trailer personnel performed mainten-
         ance and read data.

Dec.  4 - The scrubber did not operate.  The work on the 6 inch
         bleed line for the first stage was completed.  Work
         was perfomred on the mother liquor to pre-mix tank
         line and on the pH meter.  The second stellited re-
         stricting orifice plate was removed from the bleed line
         to the thickener.  An attempt was made to start the
         centrifuge but it kept tripping off.  A broken shear
         pin on the centrifuge was found.

         A new inlet probe was installed for the continuous
         monitoring trailer.

Dec.  5 - The scrubber was operated during the later part of the
         day.  The centrifuge had to be flushed with steam and
         water before it was freed.  The mother liquor to pre-
         mix tank line repairs were completed.  The pre-mix tank
         holding spring booster and the "A" second stage pump
         discharge valve were replaced.  At 1630 hours flow at
         51,200 ACFM entered the scrubber.  A second leak developed
         in the first stage discharge header.  Both leaks are


                              -C12-

-------
         in a welded joint area.  By 2130 hours the load was
         increased to 110,100 ACFM.  The recycle rate to the first
         stage dropped from 4500 gal/min. to 3500 gal/min. at
         2200 hours, but came back up by itself by 2330 hours.

         The continuous monitoring and chemical analysis trailers
         resumed analyses.

         A stearing committee meeting was held with representatives
         from EPA, Rumsford, Basic, PEPCO, Chemico and York.

Dec. 6 - The scrubber operated all day.  Early in the day the
         centrifuge cake became very wet and sticky.  A vibrator
         had to be kept on almost continually which caused low
         instrument air pressure.  At 0435 hours a large clump
         of MgO plugged up the weigh feeder.  The flow was cut
         to 117,800 ACFM because the pH started dropping.  After
         the belt was cleared the load was increased.  The flow
         was at 230,400 ACFM by 0700 hours and later increased
         as high as 240,600 ACFM.  The centrifuge hopper required
         almost constant attention due to plugging.  The grease
         fittings on the elevator belt were replaced.  All of the
         stellited orifices were removed from the bleed line to
         the thickeners because the pipe failures in this area
         were attributed to the velocity increases across the
         plates.  The DuPont SC>2 analyzer was repaired by the
         instrumentation shop.

         There were no outlet readings at 1400 while the probe
         assembly was inspected.

Dec. 7 - The scrubber operated all day.  The leaks in the first
         stage discharge header became much worse during the day.
         An unsuccessful attempt was made to patch the leaks
         with polyethylene.  At 1100  hours the load was being
         reduced in order to install a blind in the first stage
         recycle line header.  By 1700 hours the load was up to
         188,400 ACFM.  A leak developed in the spool piece in
         the first stage recycle line at the pinch valve
         location, and had to be patched.

         The continuous monitoring trailer operated all day but
         had some pump and flow problems which were corrected
         as soon as they occurred.  There were no 1500 and 1600
         hour readings because of the pump outage.

Dec. 8 - The scrubber operated all day.  The MgO weigh feeder
         belt ran off its track and had to be repaired.  An-
         other leak developed in the 6 inch spool line on the
         first stage recycle line and had to be patched.  At
         1530 hours Unit #3 had wet coal problems, and the
         scrubber load was cut to 146,400 ACFM from 188,400 ACFM.
         The centrifuge cake was still very wet and required much
         attention.

                              -C13-

-------
          The continuous monitoring trailer had some problems
          with flow on the outlet mode.  The probe had to be
          washed out, therefore the 0300 hour reading was
          omitted.

 Dec.  9 - The scrubber operated all day.  Early in the day the
          transition pipe between #1 and #2 feed screws plugged
          and the centrifuge feed was diverted long enough for
          the line to be freed.  The impeller on the "B" pump
          had to be replaced.  A piece of rubber in the north
          thickener bleed valve could not be freed so the tank
          was drained.

Dec. 10 - The scrubber operated all day.  The continuous pH
          monitor was fluctuating but this was due to the coal
          feeder problems in the plant.  New overload heaters
          of the correct rating were installed in the "B" MgO
          pump.  The rotometer for the demister spray was re-
          moved and was found to be broken and frozen.  The first
          stage recycle pumps were shut down to replace a 14 inch
          elbow.  The elbow on the 6 inch plump-bob line was re-
          moved but a new one was not installed.  A new leak
          developed in the centrifuge cover.

          The continuous monitoring trailer was operational most
          of the day.  No readings were taken from 1300 to 1600
          hours due to a sample pump outage.

          The chemical trailer performed a special study on pH
          vs. time, because of the differences between the con-
          tinuous and bench meters.  Results indicate the time
          between sampling and bench measurement was sufficient
          for the pH to increase 0.3 pH units.

Dec. 11 - The scrubber was operated only for a short time due to
          a planned shut down.  At 0300 hours new leaks were
          noticed around the patches on the first stage bleed
          line to the thickener.  The MgO tank was diluted and
          the flow was cut back in preparation for shut-down.
          At 0425 hours the I.D. fan was turned off.  The north
          thickener was allowed to finish pumping out.  The
          mother liquor pump valves were repaired and a new
          lined elbow was installed on the plumb-bob line.  The
          blind was then removed from the top of the scrubber.
          The scrubber was ready for operation at 1600 hours but
          no PEPCO operators were available for work.

Dec. 12 -• The scrubber was operated for only 2 hours today
          because a patch came off after start up.  The rubber
          was cleared from the bleed valve in the north thickener
          and refilling began.  Flue gas entered the scrubber at
          1230 hours but at 1430 a high level was noted in the
          first stage, even though the bleed valve was completely
          open.  Due to the high back pressure the patch on the
          6 inch bleed line parted.  The gas was routed out of the

                               -C14-

-------
          scrubber at this time.  The rakes on the thickeners
          were checked and found to be satisfactory.

          York Chemists were informed they would have to move
          their laboratory.

Dec.  13 - The scrubber was put on-line at 1800 hours today.  R.
          E. Donovan maintenance crews were on site in the
          morning.  A 20 foot section of 6 inch rubber lined
          pipe was installed in the first stage bleed.  The
          balance of the pipe was inspected and was found to
          have a baseball size blister in one section.  A new
          section of pipe was fabricated to replace this section.
          A test of the pumps and first stage showed there was a
          restriction between the thickeners and scrubber.  An
          inspection of a valve showed a ruptured liner.  A
          liner was used from the north thickener valve to re-
          pair it.  Gas entered the scrubber at 1810 hours at
          228,400 ACFM.  The flow was increased again at 1850
          and was at 242,200 ACFM by 2200.  The scrubber load may
          be limited as the boiler experienced wet coal con-
          ditions.  The mother-liquor agitator kept malfunctioning.
          The problem was located in the motor or gearbox.

          The York chemical lab was moved into a 36 foot trailer.

Dec.  14 - The scrubber operated all day.  A leak developed in
          the spool piece that was installed at the 6 inch pinch
          valve location on the first stage recycle line.  Main-
          tenance personnel removed the gear box from the mother-
          liquor tank agitator.  At 1600 hours the flow was cut
          to 120,300 ACFM, so that repair work to the lines
          could be performed.  At 1705 hours the load was in-
          creased again to 153,600 ACFM.

          The continuous monitoring trailer operated most of
          the day.  An electrical short caused the main sampling
          line to burn out.  A temporary replacement was installed.
          There are no 1800 to 2400 readings because of this
          electrical short.

          The move of the chemistry laboratory was completed.

Dec.  15 - The scrubber operated all day.  The centrifuge and its
          hopper had to be flushed out during the day.  A leak
          developed in the second stage discharge header.  At
          1645 hours the flow was increased to 188,400 ACFM.  At
          2030 hours the flow was cut by 48,000 ACFM because the
          MgO tank nozzle plugged up and had to be cleared.
          The flow was maintained at 140,800 ACFM for the rest of
          the day.

          The continuous monitoring trailer was semi-operational.
          The temporary sample line had intermittent freeze-up
          problems.  An insulated line was put into service in

                               -CIS-

-------
          the evening.   No readings were taken until 1400 hours.

Dec.  16 - The scrubber operated all day.  Electricians were
          called when the "B" second stage recycle pump mal-
          functioned.  They installed new overload heaters.  The
          flow was dropped to 74,800 ACFM so the welder could re-
          pair leaks in the discharge header.  At 1530 hours
          the boiler unit lost all coal feeders.  The flow was
          cut to 80,000 ACFM.  By 1840 hours the load was up to
          165,900 ACFM.

Dec.  17 - The scrubber operated all day.  Leaks developed near
          the top of the first stage vessel.  Blanks were in-
          stalled in the tangential nozzle lines to stop the
          leaks.  A new leak developed in the second stage dis-
          charge header.  During the afternoon the flow was in-
          creased to 197,600 ACFM, and a series of tests was
          carried out.

          Three York Research personnel came in from Connecticut
          to perform particle mass testing.

Dec.  18 - The scrubber operated all day.  The load was cut at
          0830 hours because of the build up of very wet
          centrifuge cake in the dryer.  The flow to the centri-
          fuge was cut at this time so leaks could be welded in
          the centrifuge cover.  A new leak developed in the
          second stage discharge header.  While loading MgSC>3,
          approximately 1 ton was spilled due to a faulty gate.
          At 1930 hours, clumps of product started coming loose
          in the dryer.  The load was cut and the centrifuge feed
          rate was reduced in order to clean the dryer.

          The continuous monitoring trailer was semi-operational.
          The SC>2 unit went off-line at 0400 hours.  The elec-
          tronics technician from York Research was in contact
          with a Thermo Electron representative throughout the
          day attempting to fix the unit.

          The stack testers from York Research performed four
          particle mass tests during the day.

Dec.  19 -• The scrubber operated part of the day.  At 1000 hours
          the second stage circulation was stopped so that
          second stage discharge header leaks could be welded.
          The gas was routed out of the scrubber at 1300 hours.
          While the scrubber was down, the dryer was cleaned with
          water.  At 1535 hours the scrubber was back on-line at
          173,000 ACFM and later flow was increased to 197,600 ACFM.
          The dryer discharge conveyor tripped and had to be reset.
          There continued to be a large build up in the dryer.

          The continuous monitoring trailer was on-line except
          for the S02 monitor.   (DuPont readings were used on the
          data sheets).  A representative from TECO was scheduled


                               -C16-

-------
          to fix the analyzer.

          No stack testing was performed due to unsteady operating
          conditions.

Dec. 20 - The scrubber operated all day.  A leak developed in the
          first stage vessel at the tangential spray nozzle level.
          The front band of rappers on the dryer were not hitting
          the drum.  Attempts to tighten the rappers were un-
          successful.  A 20 foot section of pipe to the upper pond
          developed a leak; it was replaced by a hose.

          The continuous monitoring trailer was on-line too, but
          the S02 monitor was still not working.  The CC>2 analyzer
          was down from 0600 to 0900 hours.  The TECO SC>2 unit was
          back in service in late afternoon.

          No particle mass tests were performed because the boiler
          load was too low.

Dec. 21 - The scrubber operated all day.  At 0220 hours the flow
          was increased to 130,600 ACFM.  Two leaks developed on
          stage nozzle distribution lines.  The 8 inch pinch valve
          liner on the first stage tangential nozzle line failed.

          The stack testers from York Research left today with
          plans to return in early January.

Dec. 22 - The unit was operated all day with one brief outage.
          At the start of the day, a leak developed in the first
          stage recycle line to the plumb bob on the north side
          of the scrubber.  The scrubber was taken off-line at
          0910 hours, and the pinch valve was repaired.  The
          scrubber was on-line again at 1020 hours at 140,800 ACFM.
          The flow was increased to 146,400 ACFM by 1500 hours.

Dec. 23 - The scrubber operated in the beginning of the day.
          The liner in the pinch valve of the first stage
          recycle line ruptured.  A leak also developed in a
          second stage discharge line.  The gas was diverted from
          the scrubber at 0900.

          York Research personnel departed for the holiday at
          0900 hours.

Dec. 24 - The scrubber was not operated today.  Shutdown procedures
          were completed during the day.

Dec. 25 - The scrubber was not operated today.

Dec. 26 - The scrubber came on-line at the end of the day.  The
          second stage discharge header was welded, and the first
          stage spool piece with an orifice plate was installed.
          The pre-mix tank was cleared out during the day.  An
                               -C17-

-------
          electrician was called to check a relay on the second
          stage recycle pumps.  Gas entered the scrubber at 2140
          hours.

Dec. 27 - The scrubber operated all day.  During the morning the
          load was cut so the pre-mix tank could be cleared.  A
          mechanic adjusted the packing on the first stage and
          transfer pumps.  The flow was increased throughout the
          day and was at 228,000 ACFM at 1900 hours.

          York Research personnel resumed their testing at 0800
          hours.

Dec. 28 - The scrubber operated all day.  The centrifuge had to
          be diverted so the bucket elevator and the centrifuge
          hopper could be cleared.  A leak developed on the first
          stage pump elbow and was plugged.  Leaks also developed
          in the pH meter probe assembly and second stage suction
          header.

          The SC>2 monitor in the York Research trailer was not
          working properly; DuPont readings were used from
          1700 hours on.

Dec. 29 - The scrubber was operated for part of the day.  A
          second hole on the first stage elbow had to be plugged.
          At 1000 hours the bucket elevator tripped; the inlet
          flow was reduced to allow the system to clear itself.
          At 1345 hours an upset occurred in the mother liquor
          and pre-mix tank.  The gas was routed out of the
          scrubber at this time to repair the elbow leak for a
          third time.  The ID fan would not restart because of
          a damper problem.'

          The SC>2 analyzer in the continuous monitoring was re-
          paired and on line at 1050 hours.

Dec. 30 -• The scrubber did not operate today.  Final shut-down
          operations were carried out.  The second stage suction
          header was removed, the water valve on the centrifuge
          deck was replaced, the gasket on the dryer ID fan was
          replaced, and the leaky elbow on the first stage was
          removed for repair.
                               -C18-

-------
JANUARY, 1975
      -C19-

-------
Jan. 1  - The scrubber was not in operation today.  The inside
          of the second stage was inspected and a large amount
          of crystals and dirt was found.  It was concluded
          that some of the spray nozzles were plugged.  The first
          stage elbow was replaced during the day.

Jan. 2  - Maintenance continued.

Jan. 3  - At the start of the day, maintenance was still being
          performed on the scrubber.  Two of the flow meters
          froze; replacements were ordered.  Gas entered the
          scrubber at 1545 hours and was at a flow of 266,200 ACFM
          by 2100 hours.

          A new sample line for the continuous monitoring trailer
          was installed during the day.  Leaks in fittings on the
          new line were eliminated but readings on the TECO unit
          appeared very low.  The probable cause was a bad ampli-
          fier.  Pump problems were encountered in the evening;
          therefore the readings for the day were inaccurate.

Jan. 4  - The scrubber operated until 0840 hours.  A 3 inch drain
          valve on the second stage was plugged.  The rake on
          the thickener was placed in service today.

          The continuous monitoring trailer was not in operation.

Jan. 5  •• The scrubber was not operated today.  One of the second
          stage demisters was freed, and maintenance continued.

Jan. 6  -• The scrubber was not operated today.  Maintenance
          continued.

Jan. 7  - The scrubber was not operated until late in the after-
          noon.  The second stage was inspected and found to have
          no leaks.  The valves to the second stage cone and
          tangential sprays were blocked.  The mother liquor
          agitator was repaired and re-installed.  At 1735 hours
          gas entered the first stage.  The second stage was not
          operated.  The load was increased to 255,000 ACFM and was
          up to 279,200 ACFM by 2200 hours.

          The continuous monitoring trailer had many problems.
          The sample pumps failed and part of the sample line
          burned out and had to be replaced.

Jan. 8  - The first stage was operating at the start of the day.
          At 1405 hours the gas was removed so a leak in the "B"
          discharge line could be repaired.  The first stage was
          back on-line at 1600 hours and flow was up to 180,200
          ACFM by 1700 hours.

          At 1825 the load was raised 291,800
                               -C20-

-------
          The continuous monitoring trailer operated well after
          0300 hours.  The NOx readings in the later part of the
          day were inaccurate due to a blocked capillary, which
          was discovered the next day.

Jan. 9  - The first stage of the scrubber operated until 1600
          when the load was reduced because of coal feeder
          problems.  A lubrication program was carried out during
          the day.

          The continuous monitoring trailer operated with only
          small flow problems.  The blocked capillary on the NOx
          monitor was corrected at 0900 hours.

Jan. 10 - The scrubber was operated until 0830.  The gas was re-
          moved and repairs were made on the rubber lined elbow
          on the "B" first stage pump.  A leak developed on an
          inner cone line and had to be repaired.

Jan. 11 - Repair work continued.  A leak was found in the second
          stage bleed to the centrifuge.  The first and the
          second stages of the scrubber came on-line at 1340
          hours at 146,400 ACFM.  The load increased to 197,600
          ACFM at 2100.  The centrifuge cover was leaking by the
          end of the day.

          The continuous monitoring trailer operated well, except
          that the SO2 readings for 1600 were not taken because
          the analyzer was being repaired.

Jan. 12 - The scrubber operated at a decreased load because of
          problems with the coal feeders in the station.  At
          1530 hours the MgO "A" pump suddenly lost pressure and
          the load was cut back to 188,400 ACFM; while cleaning
          and changing to the line "B" pump. The flow was then
          increased to 218,100 ACFM.  The MgO weigh feeder was
          suspected to be incorrect.

Jan. 13 - The scrubber operated at this same level all day.  Tests
          were performed to evaluate the accuracy of the MgO
          weigh feeder and it was found to be 25% high.  A first
          stage inner cone developed a leak and was repaired.  New
          leaks were noticed in the centrifuge cover.

          The continuous monitoring trailer operated all day except
          for the outlet stack temperature monitor.

Jan. 14 - The scrubber operated between 202,000 and 220,000 ACFM
          until 1640 hours when it was shut down because the MgO
          supply had been exhausted.  A number of problems were
          encountered before the shut-down.  Among them were the
          centrifuge hopper constantly plugged, the first stage
          level controller froze up, the pre-mix tank partially
          solidified, and the wash hose for the centrifuge hopper
          froze.
                               -C21-

-------
          The continuous monitoring trailer operated all day.
          No readings were taken at 0900 because the sample line
          was frozen.  This problem was immediately corrected.

Jan. 15 •• The scrubber did not operate.  The first stage was kept
          running to prevent it from freezing.  New test buckets
          were installed on the bucket elevator.  Maintenance and
          freeze-up precautions were carried out.

Jan. 16 - The first stage was again kept running to prevent a
          freeze-up.  A leak was discovered on the pH meter
          probe assembly.  Three loads of MgO arrived during
          the night shift.

Jan. 17 - The first stage was operated without gas to prevent
          its freezing.  The "B" first stage pump failed to
          work correctly and was inspected.  An 18 inch section
          of broken-off tangential spray nozzle was found in the
          pump.  A new leak developed at the 10 inch tee to the
          tangential spray.    At 1545 the first stage was shut
          down to save wear on the scrubber.

Jan. 18 - The first stage, without flue gas, was operated to avoid
          a freeze-up.  The 10 inch line with the leak was
          removed.  The ten tangential nozzles were inspected and
          the results were:  six of the nozzles were completely
          missing, two were about to break and the other two were
          in fair condition.  Because of the low plant output,
          60 MW, the scrubber could not start up until 1315 hours.
          At 1400 the load was at 197,600 ACFM.  At 1600 hours
          the dryer was fired but the screw conveyor at the top
          of the MgS03 silo kept tripping out.  The operator was
          unable to inspect the screw because of the ice on the
          scaffolding.  Flue gas was routed out of the scrubber
          at 1730 hours.

          The continuous monitoring trailer operated properly for
          the time the scrubber was on-line.

Jan. 19 - The scrubber was operated for a brief period.  The
          problem with the MgSC>3 conveyor was corrected and gas
          entered the scrubber at 1130 hours.  At 1345 the flows
          and levels in the first stage could not be controlled
          due to a plugged line.  At 1400 hours the gas was turned
          off.

Jan. 20 - The scrubber did not operate.  Maintenance was per-
          formed on a valve liner.

Jan. 21 - The scrubber did not operate.  The pumps and solids
          handling equipment were operated hourly to prevent
          a freeze-up.
                               -C22-

-------
Jan. 22 - The scrubber did not operate.  Maintenance and freeze-
          up prevention were carried out throughout the day.

Jan. 23 - The scrubber came on-line during the afternoon.  Before
          start-up work was completed on the thickener bleed line
          that plugged on Jan. 19.  Gas entered the scrubber at
          1445 hours.  At 1615 hours the flow was at 120,300 ACFM.
          Problems developed in the MgO feeder and the flow had
          to be reduced to 87,000 ACFM to maintain the pH.  At
          2245 hours the flow was raised to 99,300 ACFM.

Jan. 24 - The scrubber operated all day.  During the day leaks
          developed in the torus spray and in the first stage
          tangential spray header.  At 0630 the flow was cut to
          120,300 ACFM because of the low pH.  By 0900 hours the
          flow was increased to 207,400 ACFM.  Experiments with
          restricted flows were carried out on the second stage.
          The centrifuge hopper plugged and the load had to be
          cut to 135,700 ACFM but it was raised to 255,000 ACFM
          by 1600.  At 1650 the bucket elevator tripped.  The
          belts on the top of the elevator had to be replaced.
          The scrubber operated at 218,100 ACFM for the rest of
          the day.

Jan. 25 - The scrubber operated most of the day.  The centrifuge
          hopper was washed out to avoid plugging.  The gas was
          removed at 1500 hours to insure that the scrubber
          would be able to operate for a visit by Chemico
          management on Jan. 27.

Jan. 26 - The scrubber did not operate.  Leaks were patched and
          new belts were installed on the bucket elevator.  Pumps
          and solids handling equipment were operated hourly to
          prevent a freeze-up.

Jan. 27 - The scrubber was operated for part of the day.  Gas
          entered the scrubber at 0525 hours.  The load was
          changed many times during the day; the maximum load
          was 309,200 ACFM.  The scrubber was operated in both
          Mode I  (gas after precipitator) and Mode II  (gas
          before the precipitator).  When in Mode II it was noted
          the centrifuge cake was very dirty from carry-over
          fly ash.  At 1540 the gas was removed from the scrubber.

          The continuous monitoring trailer operated well; except
          that the inlet velocity readings before 0900 are
          inaccurate because of a crimped pitot line.

Jan. 28 - The scrubber did not operate.  Final scrubber shut-down
          procedures were carried out.

          The boiler  (Unit #3) was shut down for a major turbine
          overhaul which took several months.  The scrubber did
          not operate until August 11, 1975, when operation was
          planned for only 3 to 4 weeks to consume the MgO on hand,

                               -C23-

-------
          The supply of MgO was limited due to the shut-down of
          the Essex Regeneration Facility in Rhode Island.

Jan. 29 •- The buckets that were installed on Jan. 15th were
          removed and inspected.  They were found to be bent out
          of shape to the extent that they were ineffective.
                               -C24-

-------
AUGUST-OCTOBER, 1975
        -C25-

-------
Aug. 11 - The scrubber began operating at 1403 hours; however,
          due to the outlet damper sticking, the gas flow was
          shut off.  At 1435 gas entered the scrubber at 87,000
          ACFM.  When steam was admitted to the MgO slurry tank,
          the control valve cracked; and operation continued
          without steam.  The scrubber operated the rest of the
          day at 218,100 ACFM.

          The continuous monitoring trailer had many problems.
          Water in the gas conditioning system overflowed and
          flooded the sample lines.

          NOTE:  Due to limited manpower, scrubber operating
                 parameters were taken only every 2 hours.

Aug. 12 - The scrubber operated all day except for a brief shut-
          down.  The outage was to replace some first stage bleed
          lines.

          The continuous monitoring trailer experienced more
          flooded lines because the condensers failed during
          the night.

Aug. 13 - The scrubber operated most of the day at between 197,600
          and 218,100 ACFM.

          The continuous monitoring trailer was off line because
          of the problems with excessive moisture in the sampling
          lines.

Aug. 14 - The scrubber operated all day.  At the start of the day,
          the flow was cut to 120,300 ACFM and then further
          reduced to 82,900 ACFM because of a build up of dryer
          product.  By 2400 hours it had been raised to 180,200
          ACFM.

          The continuous monitoring trailer was not on line because
          of gas conditioner malfunctions.

Aug. 15 - The scrubber operated for only a short time today.  The
          flow was increased to 207,400 ACFM by 0225 hours.  Because
          of a build up of the dryer product, the flow was reduced
          and at 0400 the scrubber was shut down.

          Repair work continued on the continuous monitoring
          trailer.

Aug. 16 - Repair work was initiated oh the dryer drum.  The boiler
          developed a tube leak at 0018.  Repairs on the boiler
          tube were complete at 2010.

Aug. 17 - Repair work on the scrubber continued.

Aug. 18 - Repair work on the scrubber continued.
                               -C26-

-------
Aug. 19 - Repair work on the scrubber continued.

          Air conditioning maintenance people repaired the
          condensing units on the continuous monitoring sample
          system.

Aug. 20 - Repair work on the scrubber continued.  The boiler
          developed a reheater tube leak at 0100.  This was re-
          paired by midnight.

Aug. 21 - Repair work on the scrubber continued.

Aug. 22 - Repair work on the scrubber was completed.  Gas entered
          the scrubber at 1430 hours at 153,600 ACFM.  The flow
          was raised to 197,600 ACFM by midnight.

          The continuous monitoring system operated well after
          start up.

Aug. 23 - The scrubber was at a flow of between 197,600 and 228,400
          ACFM for most of the day.  At 1800 hours the bucket
          elevator tripped several times but was finally restarted.
          At 2300 hours, centrifuge clogging problems forced a
          scrubber shut-down.

          The continuous monitoring trailer was shut down at
          0500 because of moisture problems.  The outlet mode
          only was operational from 1600 hours.

Aug. 24 - The centrifuge hopper was washed out.

Aug. 25 - The centrifuge cleaning and repair was completed.  Gas
          entered the scrubber at 1330 at 173,100 ACFM.  By 1600 the
          load was increased to 180,200 ACFM.

          Air conditioner repair people serviced the conditioning
          units on the continuous monitoring trailer.  The outlet
          mode was operational at start up and the inlet mode
          on-line at 2200 hours.

Aug. 26 - The scrubber was operated until 1830.  At this time
          it was decided to  shut the second stage down and adjust
          the weir height in the centrifuge.  It was hoped that
          this would produce a dryer centrifuge cake.  The first
          stage was operated the remainder of the day.

          The continuous monitoring system operated all day.  At
          2030 hours it was  placed on outlet mode only for the
          night.

Aug. 27 - The first stage of the scrubber operated until 1530
          hours when it was  taken off line to repair leaks in
          the first stage recycle lines.


                               -C27-

-------
           The continuous monitoring trailer operated on outlet
           mode only until 1200 hours.  Repairs on the inlet
           conditi cner were completed and inlet/outlet monitoring
           resumed.

 Aug. 28 •- Shut-down procedures were carried out on the scrubber
           and continuous monitoring trailer.

 Aug. 28-
 Sept. 11  Repairs on scrubber continued.

Sept. 11 -• Scrubber operation was limited to the first stage in
           order for the plant to conduct a study on particle re-
           moval using both the electrostatic precipitator and the
           scrubber.  The first stage began operation at 0925 and
           shut down 12 hours later for repairs on the boiler and ESP,

Sept. 12 -
Sept. 18   Particle removal study continued.

Sept. 19 - Repairs planned on stirrer bearing on MgO slurry tank
Sect  20   agitator.  First stage in operation for a total of 84
  p *      hours during study

 Oct. 19 - Wait for delivery of bearing.

 Oct. 20 - Scrubber startup of both stages.  The centrifuge was com-
           pletely "cemented" with product and during the startup the
           pins were sheared.  Maintenance and further repair of the
           unit was judged too costly by the plant representatives
           and the program was terminated.
                                  -C28-

-------
APPENDIX D
METHODOLOGY
     -Dl-

-------
-D2-

-------
CHEMICAL ANALYSES
   METHODOLOGY
       -D3-

-------
% FREE WATER ON CENTRIFUGE CAKE

A portion of the sample was weighed in a tared vessel.  Several
aliquots of acetone were added to wash the sample which was stirred
and separated.  The sample was transferred to a tared watch glass,
oven-dried for 30 minutes and re-weighed to obtain the oven-dried
sample weight.


     Calculation:  % Free water = 100 - % solids

     where:        % Solids = wt. of oven-dried sample
                              wt. of original sample


% COMBINED H?0 on CENTRIFUGE CAKE AND DRYER PRODUCT

A 10.0 gr  portion of the oven-dried sample was placed on an
OHAUS moisture balance for 50 minutes.  When complete, % moisture
was read from the calibrated scale.
pH

The pH of the samples was taken using a Corning Research pH
meter.  The meter was first standardized using two standard buffer
solutions; and temperature compensated.  Readings on the meter were
then takein + 0.01.
DENSITY DETERMINATION ON MOTHER LIQUOR, 2nd STAGE BLEED, MgO SLURRY

A 10.0 ml   (2 ml ) sample was placed in a tared graduated tube
and weighed on an analytical balance.  This analysis was always
performed in triplicate.


     Calculation:  wt. sample  = Density in  ms/ml
                   ml  sample


APPARENT DINSITY;  CENTRIFUGE CAKE AND DRYER PRODUCT  (As Received)

A 100 ml  plastic cup was tared and filled loosely with sample to
the mark.   The weight was taken on the triple beam balance and
evaluated:
     grans/100 ml = weight/100 ml

SUSPENDED SOLIDS (mq/1)

200 mis of sample filtered through a tared millipore filter, dried
in an oven for 1 hour @ 125°F and weighed.

     Calculation:  mg/1 S.S. = mgs S. solids  x 5
                               200 mis sample

                                -D4-

-------
% MgO IN MOTHER LIQUOR, MgO SLURRY AND SECOND STAGE BLEED

A portion of the sample was collected into a graduate centrifuge
tube.  The exact volume was noted and the sample was analytically
transferred to a beaker.  A reaction with 3% H202 was induced by
boiling and a quantity of H2SC>4 was added.

     For MgO slurrys add 25 ml of 2.512N H2S04

     For Mother Liquor, 2nd stage bleed add 10 ml of 2.512N H2S04

The solution was stirred and boiled for 5 minutes, then diluted.
When cooled, a methyl purple indicator was added and the solution
was titrated with NaOH to a distinct green endpoint.

     Calculation:  % MgO =  (ml H2S04 x N) -  (ml NaOH x N)
                                    mis sample

% MgO DETERMINATION ON CENTRIFUGE CAKE  (OVEN DRIED) , DRYER PRODUCT
2nd STAGE BLEED SOLIDS, MOTHER LIQUOR SOLIDS, MgO BELT

These samples were prepared as above except the quantity of
H2S04 which was added.

     For MgO Belt sample add 25.0 ml of 2.512 N H2SO4

     For the rest add 50.0 ml of 0.50 N
     Calculation:  % MgO =  (mis H?S04 x N) -  (mis NaOH x N)   0 n, ,
                             1             i   — .-"             JC £• • \) J. 0
                                      sample wt.
CHLORIDE
     Liquid, Homogeneous

     A portion of the sample was treated with an aliquot of HN03
     and AgN03 and allowed to become turbid.  The concentration
     of chloride was calculated from the turbidimetric calibration
     curve, FIGURE D-l and the turbidity reading on the meter.

     Solids and Slurrys

     A weighed sample was treated with an aliquot of HN03 and
     heated to complete dissolution.  The contents were then
     diluted to a known volume and an aliquot was treated with
     AgN03 .  The resultant turbidity was read on a meter and
     calculated from the calibration curve, FIGURE D-l.

          Calculation:  % Cl- = mg/1 x vol.
                                       rooo x
                                  wt. x 1000
                                -D5-

-------
 I
a

-------
Percent Magnesium

The percent magnesium was determined by a titration with a
standard solution of disodium ethylenediaminetetraacetic
acid solution (EDTA).  The pH was adjusted to 10 + 0.05.  A
suitable sample volume was chosen, the pH adjusted and titrated
with EDTA solution.  The end point of the titration was deter-
mined by the addition of Eriochrome Black T, because the
indicator color was red in the presence of magnesium and blue
when the cations are completely complexed with the EDTA.
Calculations were made from the amount of titrant consumed
by the sample.  The amount of magnesium was determined on the
filtrate portion of the samples.  Calcium was first precipi-
tated out of solution as the oxalate.  The magnesium was
calculated from the amount of EDTA consumed and reported in
gr/1.

Magnesium content in solids was determined by treating a
weighed portion of the sample with 1:4 HNC>3 and heated until
dissolution was complete.  The solution was then diluted and
an aliquot treated with NH4O4, oxalic acid and filtered.
The solution was buffered to a pH of 10.0 + 0.02 and titrated
as above.

     Calculation:  % Mg = mg/1 x vol.  x IQO%
                          	1000	
                              wt. x 1000


% SOLIDS (GRAVIMETRIC) ON 2nd STAGE BLEED AND MOTHER LIQUOR

An aliquot of the sample was placed in a preheated, tared
bottle and weighed.  The sample was shaken, filtered, and
re-weighed.  The filter was then washed repeatedly with
portions of acetone and dried in an oven at 135°F for 30
minutes.  The sample was then re-weighed and calculated as
follows:

     % Solids = wt. dry solids   ,nn
                — —   <\—   ,     X -L U U
                  sample wt.

% MgSOa on 2nd STAGE BLEED FILTRATE

The filtrate saved from the % solids analysis was allowed to
sit for 1-2 hours to allow any solids to settle out.  10.0
mis was pipetted into a tared vessel, and weighed.  From this
the density equalled 0.1 x weight of 10 ml.

Calculation:  The % MgSO^ is then read from the graph on the
following page  (data from Perry's Engineering Handbook).
(Figure D-2)
                           -D7-

-------
 I
o
oo
 I
                 2S  -
                20
                 5  '
                                                                                           DENSITY OF

                                                                                                  SOLUTIONS


                                                                                           (ref.  Perry's Handbook)
                  1 .0(1
1.05       1.10       1.15      1.20

                           Density
1.25
1.30

-------
     Sulfate

     Sulfate was determined on a filtered sample because
     particulate matter interferes with the gravimetric
     method.  Determinations made on solid samples were per-
     formed after the potassium carbonate fusion (1.2) and
     dissolution.  The clarified sample was acidified to a
     pH of 4.5-5.0, an additional amount of hydrochloric
     acid was then added.  This solution was heated to boil-
     ing and, while being stirred gently, a solution of
     barium chloride was added slowly until precipitation
     appeared complete; then a 2 ml excess of barium chloride
     was added.  The precipitate was digested at 80-90°C,
     and to insure proper crystallization of the BaSC>4 the
     solution was let to stand overnight.  The precipitate
     was filtered and washed with distilled water until free
     of chloride.  The BaSC>4 crystals and the filter were
     dried and ignited at 600°C for one hour, cooled in a
     dessicator and weighed.  The amount of sulfate present
     in the sample was calculated from the equation:

          mg 804/1 = mg BaSO* x 411.5
                       ml of sample
% MgS04 in DRYER PRODUCT, CENTRIFUGE CAKE  (OVEN-DRIED) AND
MgO BELT SAMPLES

A weighed portion of sample was diluted and treated with an
aliquot of 1:1 HC1 and boiled for several minutes.  The hot
solution was filtered analytically.  A portion of the cooled
solution was treated with a HACK Sulfaner reagent and placed
in a colorimeter cell.  The solution was allowed to react
and then shaken.  The absorbance was then read on the color-
imeter, and calculated from the calibration curve (Figure D-3)

     Calculation:  % MgS04 = meter reading x 0.3133
                           -D9-

-------
o
I
           125
           100
        3
        3
        (A
                                                               -H44-4--W4WW  -H-J4I H
                                                                          SULFATE

                                                                          BY

                                                                          SULFAVER IV
                                                                                      30    40    50   60  70  80 90 100

-------
% MgS03 IN CENTRIFUGE CAKE AND DRYER PRODUCT

The percent sulfite in the solid samples was determined titri-
metrically.  A weighed portion of the sample was treated with a
normal solution of sodium and diluted with water.  Immediately
before titration with 0.1N solution of sodium thiasulfate, an
aliquot of 1:1 HC1 was added.  The solution was titrated to a pale
yellow and a few drops of starch indicator added.  The titration
continued until a clear endpoint was obtained.
     Calculation:  % MgSOj =  (ml 12 x N l2)-(ml Na2S;)03 x NH  S?C>3)x5.215
                                           sample wt.


% MgS03.6H2O in SECOND STAGE BLEED AND MOTHER LIQUOR

A portion of the sample was collected in a graduated centrifuge
tube and the exact volume noted.  The contents were transferred
analytically, diluted, and treated with 2.5 normal H2S04 dropwise
to a pH of 4.5-5.0.  An aliquot of Kl-starch indicator was added
and the solution titrated with standard KI03 solution to a faint
blue color.  The solution stirred with a magnetic stirrer and
titrated carefully to a deep blue endpoint.

     Calculation:  % MgS03.6 H2O = ml KIO3 x NKI03 x 7 . 08
                                        ml sample

     % Sulfite

     As above with the following calculation:

          %S03 = ml KI03 x NKI03   x 2.668

                       ml sample
                                -Dll-

-------
-D12-

-------
CONTINUOUS MONITORING
SAMPLING PROCEDURES AND
WET TEST RESULTS
          -D13-

-------
MONITORING HARDWARE

The mobile emissions measuring laboratory consisted of six
separate monitoring devices for continuous 24 hour measurement
of sulfur dioxide, nitrogen oxides, carbon dioxide, carbon
monoxide, oxygen, and inlet velocity pressure.  Each unit was
selected for its accuracy, reliability, and applicability.  In
addition to these units, inlet duct, outlet duct and sample
line temperature were monitored with chromel-alumel thermocouples
and digital readouts.  All of the above systems had Rustak strip
chart recorders operating continuously.  A brief description of
each of the emissions monitoring instruments follows.
                                -D14-

-------
THERMO-ELECTRON CORPORATION MODEL 10B CHEMILUMINESCENT NO-NOX
                            ANALYZER
The TECO NO-NOX Gas Analyzer provides a sensitive and accurate
means of continuously measuring the concentrations of nitric
oxide (NO) and total oxides of nitrogen (NO + N©2) in stack
gases.  The heart of the analyzer is the cylindrical reaction
chamber Figure D-4 where sample gas containing NO molecules
mixes with 03 molecules from the ozone generator.  Electronically
excited N02 molecules are created which emit light (chemilumines-
cense) as the orbital elecrons decay to their ground state.
Specifically:

               NO + 03	*• N02 + 02 + hj/

In operation, dry filtered air is drawn into the instrument and
a portion is converted to 03 in an ozone generator.  Separate
capillary tubes carry the mixture of 02 and 03 and sample gas
into the reaction chamber where mixing occurs.  A vacuum pump
keeps the reaction chamber pressure at a constant -25 inches of
mercury.  The chemiluminescent signal in the reaction chamber is
deflected by a high sensitivity photomultiplier tube; the de-
flection of which is limited to the narrow wavelength band pro-
duced only by the NO-03 reaction.  The signal as it leaves the
tube enters an electrometer amplifier which further amplifies
the signal and converts it to voltage.  The amplifier voltage
output powers the meter and the strip chart recorders.

To measure NO concentrations, the sample gas to be analyzed is
blended with 03 in the reaction chamber.  The resulting chemi-
luminescence is monitored through an optical filter by a high
sensitivity photomultiplier position at one end of the reactor.
The output from the photomultiplier is linearly proportional to
the NO concentration.

To measure NOX concentrations the sample gas is diverted through
a stainless steel heated coil which converts any N©2 to NO before
the sample enters the reaction chamber.  The chemiluminescent
response is linearly proportional to the NOX concentration
entering the converter.
                                -D15-

-------
                     EXHAUST
                                          NO MODE
                                FILTER
DRY AIR
  OR
OXYGEN
                      PHOTO-
                     MULTIPLIED
                                                              NO OR NO
                                                              SAMPLE
            NOX - NO
           .CONVERTER
                                           NOX MODE
           STRIP CHART
            RECORDER
            (OPTIONAL)
POWER
SUPPLY
                          FIGURE D-4

   Chemiluminescent NO-NOX Gas Analyzer Conceptual Schematic
                                -D16-

-------
INSTRUMENT CALIBRATION

All analyzers were calibrated daily in the manner specified by
the manufacturer of the instrument.  Calibration Gas was stored
in the rear of the York Research Corporation Monitoring trailer
and was injected at specifically controlled rates from the
master control panel located within the trailer proper.

In addition to the standard calibration methodology, the
combination gas was injected up an auziliary sample carrying
line into the probe and then returned to the analyzers through
the usual passageways.  Utilizing this method, York engineers
could determine if probe or sample line leakage existed.

As a final check on the instruments, York Research performed
wet chemical testing under strict EPA guidelines (Tables D-l
through D-5) .  Samples were taken simultaneously at the inlet
position and the trailer's analyzer lead-in, and then again at
the outlet position and the trailer's analyzer lead-in.  The
following methods were used to verify instrumentation:

Sulfur Dioxide:  EPA Method #6
Nitrogen Oxide:  EPA Method #7
Carbon Dioxide, Oxygen, and Carbon Monoxide:  EPA Method #3
The S02 sampling and analysis was performed in accordance with
the specifications outlined in the Federal Register, Vol. 36,
No. 247 - Thursday, December 23, 1971, and designated as Method
6 - "Determination of Sulfur Dioxide Emissions From Stationary
Sources".  This method basically consists of pulling the stack
gas sample through a heated, glass-lined probe and bubbling it
through a series of four midget impingers, reference Figure 1.

The first impinger contains 15 ml of isopropanol, which will
scrub the SOj and ^304 out of the sample gas stream.  The next
two impingers each contain 15 ml of hydrogen peroxide, which
is used to oxidize the S02 to S03 and react with the 503 to
form H2SO^j.  The fourth impinger remains empty.  The S02 samples
were analyzed on-site by titration to a pink end-point using
standardized barium chloride.

Nitrogen Oxides

Nitrogen oxide samples were taken using Method 7 - "Determination
of Nitrogen Oxide Emissions From Stationary Sources" as printed
in the Federal Register, Vol. 36, No. 247 - Thursday, December 23,
19-1.  The procedure for obtaining the sample is to evacuate a
two liter glass flask to approximately 26 inches of mercury.
The flask, containing 25 ml of a sulfuric acid - hydrogen
peroxide solution, is evacuated and leak- tested.  Stack gas is
then pulled into the flask by vacuum and a complex of H2S04/N02
                                -D17-

-------
is formod.  Any NO that is present in the stack gas is oxidized
to N02 with available oxygen from the hydrogen peroxide.  See
Figure !>.

Analysis of the sample is performed by reaction with phenoldi-
sulfonic acid in a basic medium.  A yellow nitrate is formed
which has a color proportional to the concentration.  The ab-
sorbanco is then read by a spectrophotometer at 400 nm.
                                -D18-

-------
              TABLE  D-l.   EMISSION TESTING WITH CONVENTIONAL EQUIPMENT
Date
11-26-74




12-6
12-9
12-10
12-14
12-17
12-18
12-19
12-8





12-18
12-20
12-21
1-7-75
1-8-75
1-9-75
1-10-75
Parameter
S02
so2
02, C02 and CO
TT
TI
S02
so2
S02
so2
S02
so2
so2
02 and C02
TT
n
TT
TT
t!
4 particulate mass
2 " it
2_ it IT
so2
S02
so2
so2
Location
Outlet (Duct)
Outlet (Trailer
Outlet (Duct)
Outlet (Trailer)
Outlet (Instruments)
Inlet/Outlet
Inlet/Outlet
Inlet
Inlet/Outlet
Inlet/Outlet
Inlet
Inlet/Outlet
Inlet (Duct)
Outlet (Duct)
Inlet (Trailer)
Outlet (Trailer)
Analyzer (Inlet)
Analyzer (Outlet)
Inlet/Outlet
IT
tT
IT
TT
H
TT
Method
EPA # *
6
6
3
3
3
6
6
6
6
6
6
6
3
3
3
3
3
3
5
5
5
6
6
6
6
* Fcick-ral Resistor. Doc. 23, 1971, Vol. 37, No. 247
                                    -D19-

-------
 TABLE D-2.  WET CHEMICAL VERIFICATION OF INSTRUMENTS
S02 - EPA Method 6, 11/26/74

1300:  Outlet at Duct     -  170 ppm
       Teco Model 40      -  150 ppm

1330:  Outlet at Trailer  -  161 ppm
       Teco Model 40         150 ppm
0;>, C02, CO - EPA Method 3, 11/26/74


                                % 02   % C02      %CO
1400:


1430:


Inlet at Duct
Inlet at Trailer
Inlet at Instruments
Outlet at Duct
Outlet at Trailer
Outlet at Instruments
6.5
6.6
6.2
8.0
8.0
7.9
13.8
13.5
13.6
12.5
12.4
12.6
0.0
0.0
0.0
0.0
0.0
0.0
                         -D20-

-------
TABLE D-3.  INSTRUMENT CALIBRATION - JANUARY 1975
Date
1/8/75
1/10/75
1/11/75
1/12/75
1/14/75
1/24/75
1/25/75
1/27/75
Type of
Time Reading
0840 Desired
Actual
Difference
0025 Desired
Actual
Difference
1200 Desired
Actual
Difference
0025 Desired
Actual
Difference
0125 Desired
Actual
Difference
Desired
Actual
Difference
0505 Desired
Actual
Difference
0525 Desired
Actual
Difference
S02
(ppm)
1000
1000
1000
1000
1000
1000
1000
910
-90
1000
1000
1000
1100
+100
1000
1000
1000
950
-50
(ppm)
520
620
+100
500
540
+40
520
520
500
500
520
515
-5
500
500
500
420
-80

CO2
15.0
14.0
-1.0
15.0
13.5
-1.5
15.0
15.0
15.0
16.0
+1.0
15.0
14.0
-1.0
15.0
15.0
15.0
11.0
-4.0

*2
5.0
6.2
+1.2
5.0
4.8
-.2
5.0
5.0
5.0
5.0
5.0
5.0
5.0
4.9
-0.1
5.0
5.0

                        -D21-

-------
           TABLE D-4.  GAS ANALYSES - EPA METHOD #3*
              December 8,  1974  Time;  1415 hrs.
Location
::nlet
Duct
Outlet
Duct
Trailer
Inlet
Trailer
Outlet
Analyzer
Inlet
Analyzer
Outlet
% C02
12.0
12.0
12.3
11.8
11.5
11.5
12.0
12.0
11.8
11.8
11.8
11.5
12.5
12.7
% 02
6.0
6.5
5.5
6.0
6.5
6.8
6.5
6.5
5.5
6.3
6.5
6.8
6.5 (1500 hrs)
6.8 (1400 hrs)
* Federal Register (Vol. 37, No. 247, December 23, 1971)
                               -D22-

-------
TABLE D-5.  SC>2 WET TESTS  -  EPA METHOD #6*



Date
12/6
12/9
12/10
12/14
12/17
12/18
12/19
*

**
***
****
ppm
S02
Wet Test
Time Inlet
1200 945
1000 1030
1300 1166
0300 1185
0300 833
0200 ***N
0500 1122
Method 6 - Federal
December 23, 1971)
Leak in main sample
Not in service
Not sampled
ppm
SO 2
Wet Test
Outlet
154
270
N
228
122
132
193
Register,

line


X
ppm N ppm
DuPont
In
***
1020
—
1140
840
N
1140
(Vol.




Out
*
234
N
216
132
156
204
37, No




TECO
In
930
VL050
800**
1200
800
N
^"
. 247,




Out
145
'(220^
N
230
130
150
^





                   -D23-

-------
              TABLE D-6.  WET TESTS - JANUARY 1975
Date

1/7/75
1/7/75
1/7/75
1/8/75
1/9/75
1/10/75
Time

0330
0600
2300
1830
0200
0400
SO 2 ppm
Wet*
Inlet
1042
1137
1147
1286
892
791
SO 2 ppm
TECO
Inlet
1050
1160
1160
1300
900
800
SO 2 ppm
Wet*
Outlet
126
1140
1032
1299
824
716
SO 2 ppm
TECO
Outlet
133
1160
1040
1320
825
700
* Metho3 6 - Federal Register (Vol. 37, No. 247, Dec. 23, 1971)
                               -D24-

-------
     APPENDIX E
TRANSIENT CONDITIONS
          -El-

-------
                                 SlirMAKY OF BOILER RELATED TRANSIENT  CONDITIONS
Condition
                    Pre-     Tran-            Pro-    Tran-             Pre-      Trnn-
                    vious    sient            vicnis*  sient             vious*    sient
       Ihir.itJon     SOj In-  Coud.            S02     Cond.             % S02     Com!.
       of Tran-     lot      SOj In-   %      Outlet  SOj Out-  %       Removal   ?< SO^
Date   sicnt Coml.  (ppm)    let (ppm)  Change  (ppm)  let (ppm) Change   Efficency Kcm.Ef F.  Chang





1
w
ro
I







D rop in
Boiler load
wet conl
Rising
Boiler
Load

Coal Feeder
Problem
Wet Conl
Coal Feeder
Problem

Coal Feeder
Problem
in SO in SO
f™:isoo.
1.2/8 12/8-12/9 080 1109 + 13% 1.'I3 273 + 91°* 85. U
I'l hrs.
(O'IOO-2'IOO,
12/9 12/9) 1109 925 - 10. tt& 273 207 -2'l% 75.3

21 hrs.
(2300-2000,
12/20 12/20) 1269 IOGO -16.5% 232 232 - 81.7
2 hrs.
12/17 (0800-0900,
12/17) Rl'l 78S -.1.0% 12U 183 +'17.696 8M.7
10 hrs.
1712 (2UOO-0900,
in
Eff .
75. T -10.1%


77. f. +2.3*



78.2 -3.556


75.7 -9.0*


1098
+-9.09^
                                                111    155
+9.9"/
                                                                          85.8
                                                                                                85.8
*  Previous refers to steady state conditions existing before the  transient condition.

-------
               .Condition
                                      Date
W
U>
 I
                Centrifuge Repair     Ll/lS/VU


                Centrifuge Diversion   l/l't/75


                Centrifuge
                  Diversion           12/28/7'(

                1st  Stage Outage      .12/7/74
2ml Stage Outage     12/16/7'»


2nd Stage Outage     12/19/7 4


Drop in boiler load  12/8/74




Rising Boiler Load   12/9/74

Boiler feed problem  12/20/7'»
          TRANSIENT CONDITIONS - CAUSES

                  Cause

Cover leak - abrasive matorial in centrifuge
feed wearing on the carbon steel

Maintenance procedure - wash out the clwte
to prevent clogginy

Clogged hopper - wet centrifuge cake,
possibly due to improper weir height

Leak - 1st Stage recycle lines.  Breaks in
rubber lining exposed carbon steel pipe to
low pU/high abrasive content liquid of 1st
stage

Leak in discharge heailer - abrasive action
of the solids laden slurry

Repair recycle header - 20" pipe very thin
due to abrasive action; holes easily formed

Wet coal - high surface moisture that
reduced pulverized mill outlet temperatures
to below the 1SO°F minimum needed to main-
tain an adequate drying cake.

Partial alleviation of wet coal problem

Wet coal - agglomeration of coal particles
before the pulverizer
                                                                                   Scrubber Operator Response

                                                                                 Reduction in fan rpms and MgO
                                                                                 slurry feed flow
                                                                                 None
                                                                                 None

                                                                                 Initial  reduction of fan rpras
                                                                                 (1 hr.), and -then complete
                                                                                 first stage shutdown
Tan rpms reduced and complete
second stage sliutdown

Fan rpms reduced and complete,
second stage shutdown

Boiler operators reduced fan
rpms
                                                                                                Fan rpms increased
                                                                                                Fan rpms reduced

-------
                 DURATION OF TRANSIENT CONDITIONS
                                Duration of
                                Transient
                              Period  of
Condition
Centrifuge Repair
Centrijfuge
Diversion
Centrifuge
Diversion
1st Stc.ge Outage
2nd Stage Outage
2nd Stage Outage
Date
11/15/74
1/14/75
12/28/74
12/7/7 U
12/16/74
12/19/74
Condition
2 hrs. 40 min.
for repair
< 1 hr.
< 1 hr.
SO min. actual
outage time
1 hr. 15 min.
outage time
3 hrs. of 2nd
Emission Influence
5% hrs.
-0-
-0-
3 hrs.
3 hrs.
Stage
2nd Stage Outage     8/26/74
Drop in boiler
load-wet coal        12/8/74
Rising Boiler Load   12/9/74
           outage, then complete
           scrubber shutdown for
           2 hrs.                 6 hrs.

            y 6 hrs., 2nd stage
           out until end of
           testing on Aug. 27     > 6 hrs.
           2'l hrs.
           2 hrs. for boiler
           load to reach
           previous levels
Coal Fee'der
Problem

Coal Feeder
Problem
Boiler Feed
Problem - Wet
Coal
12/17/74


VI2/7 5
2 hrs.
 > 24 hrs. before
boiler load back
to previous levels
12/20/74   21 hrs,
                      24 hrs. - rising
                      boiler load
                      followed

                       > 48 hrs.
                      before gas flow
                      and efficiencies
                      back to previous
                      levels
3 hrs.
0 hrs.;  no
adverse effect
on unit operation
                       > 24 hrs.
                                 -E4-

-------
           * RANK OF TRANSIENT CONDITIONS - EMISSION INFLUENCE
Inducing Greatest
Efficiency Drop

1.  Second Stage
Outage 8/26/75

2.  Second Stage
Outage 12/16/74
3.  Drop in boiler
load - wet coal
12/8/74
Longest Duration of
Emission Influence

1.  Drop in boiler
load - wet coal
12/8/74

1.  Boiler Feed
Problem - Wet Coal
12/20/74

3.  Second Stage
outage 8/26/75
4.  Centrifuge Repair   4,
11/15/74

5.  Coal Feeder Problem 5.
12/17/74
6.  First Stage Outage
12/7/74
    Centrifuge Repair
      11/15/74
                    Combined Ranking

                    1.   Second Stage
                    Outage 8/26/75

                    1.   Drop in boiler
                    load - wet coal
                    12/8/74
                    3.   Second Stage
                    Outage 12/16/74
                    4.   Centrifuge Repair
                        11/15/74
    Second Stage Outage 5.  Boiler Feed
    12/16/74            Problem -Wet Coal
                        12/20/74
5.
First Stage Outage
12/7/74
7.  Boiler Feed Problem 5.  Coal Feeder Prob-
Wet Coal 12/20/74       lem 12/17/74
6.  Coal Feeder
Problem 12/17/74

7.  First Stage
Outage 12/7/74
   Excluded from the table is the transient condition that posi-
   tively affected scrubber performance - the rising boiler load,
   and those that demonstrated negligible effects;   The two brief
   centrifuge diversions; the leak of the first stage discharge
   header before its repair; the coal feeder problem on 1/12/75;
   and the second stage outage of 8/26/75, when inadequate data
   prohibited a proper assessment of its consequences.
                                 -E5-

-------
BO.lLIiiR/SCRUBUER  DATA jM/KlNs: IRAN'S] liNT CON'UmoNS
Date 11 November 74 Timn Span 0100-0245 n-ansient LoncUtion 31lut Duwil "










i
w
(Tv
1


Time
0100
0115
0130
0145
0200
0215
0230
0245



Boiler Scrubber A F
Load 2nd Stage
(MK) fin. I!?0)
5.1

5.1

1.0

o.o




1 Scrubber Inlet
Inlet Srrubber SO?
ACFM pll fpp.-,}
6.5 1000

1000
6.0
1175

5.6 1200




Outlet
S()2
(ppirO

220

220

250

1200



Leaks
SO? Removal
Ei'rieier.cy
"f -

78.0

78.0

78.7

o.o




-------
                                  BOILKR/SCRUBBCR  DATA DURJNC TRy\NSIENT CONDITIONS
I
W
-j
I
Date 12 November 74 Time Span  1900-2000    Transient Condition Shut down - broken belt on
                                                               Dryer
                                      Scrubber
                                       Inlet
                                       ACFM
Tijne

1900
1915
1930
1945

2000
                        Boiler
                         Load
                          fMW)
Scrubber   P
2nd Stay;e
fin. H?6)
Scrubber
   Pll
                                                          Inlet
                                                           SU2
Outlet
 S02
 (ppr,i)
                         188
                         185
                            7.1
                            7.0
                                                                         920

                                                                         900
SOp Removal
Efficiency
                      185

                      150


                   OFF SCALE
                                                            80.2

                                                            83.3

-------
                                      DATA Ul'K I \(; TRANS HA'T CONDITIONS
Date 15 November 71* Time Span 0940-1300 Transient- Condition C.c
Roller Scrubber A. P Scrubber Inlet
Load 2nd Stage Inlet Scrubber S02
Time (MW) fin. HI") ACFM pH (,,pm)







i
n
00
1




0930
0945
1000 180 5.8
1015
1030
1045
1100 3.0
1115
1130
1145
1200 178 3.0
1215
1230
1.245
780

6.4 1150

1450

7.3 1300

1200

7.1 1100

in so

JTtrij.ugc Rt
Outlet
Cppm)

100

250

340

340

27!)

265

210
-uair

SOp Removal
Efficiency

87

78

76

73

77

75

80

.2

.3

.6

.8

.5

.9

.0
1300
5.0
7.3
1050

-------
Bmhr.K/SCKl'BHCR DATA  DTK IMC TRANS! r.\!'J' COM) ITTONS
Date 16 November 74 TiiTie Span 1930-2145 Transient Condition Shut Down- leaks









i
W
vo
I



Time
1930
1945
2000
2015
2030
2045
2100
2115
2135
2145
Boiler Scrubber /^ P Scrubber Inlet
Load 2nd Stage Inlet Scrubber S()2
(MW) fin. H?0) ACFM pi I fnpnO
1000

178 1.2 — 7.4 1000

1000

7.4 1000

0.0 — 1000

Outlet
S(>2
fppn)

230

250

210

210

1000
SOo Removal
Efficiency
• u

77.0

75.0

79.0

79.0

0.0

-------
BOILCR/SCRUniJCR DATA DUKJNC TRANSJCNT CONDITIONS
Date 24
Time
0240
0300
0315
0330
0345
0400
i 0415
« 0430
0
i
November 7 4 Time Span 0240-0430 Transient Condition Start-Up
Boiler
Load
(MW)

148



150




Scrubber A.
2nd Stage
Tin. H?0)

0.5
'£*. b


2.5

2.5


P Scrubber. Inlet
Inlet Scrubber S02
ACFM PH (ppm)

7.7 800

850
'
7.7 875

875


Outlet
S02
(ppm)
170

150

150

240



SOp Removal
Efficiency
78.8

82.4

82.9

72.6



BOILER/SCRUBBER DATA DURING TRANSIENT CONDITIONS
Date 24
Time
•MMMHM*
0730
0745
0800
0815
0830
0845
November 74
Boiler
Load
fMW)


147



Time Span 07
Scrubber ^
2nd Stage
(in. H?0)
4.9
6.8
5.5
6.4
0.0

30-0845 Transient Condition
^P Scrubber. Inlet
Inlet Scrubber 803
ACFM pH (ppm)
900

7.3 900

850

Shut-Down
Outlet
S02
(ppm)

190

190

850

SOp Removal
Efficiency

78.9

78.9

0.0

-------
                    BOILER/SCRUBBER DATA Dl:K!\C TRANSIENT CO\'DITIONS
Date 1 December 7 4 Time Span 1800-2200 Transient Condition Scrubber Shut
Boiler Scrubber ^ P Scrubber Inlet
Load 2nd Stage Inlet Scrubber S02
Time (MW) (in. H?0) ACFM pH (ppm)







i
w
i





1800 178 6.2
1810
1820
1830
1840
1850
1900 176
1910
1920
1930
1940
1950
2000 177 5.4
2010
2020
2030
2040
2050
7.1
900

900

900

880
850
7.1 900
850

880

Outlet
S()2
(ppm)
200

205

200

200
210
210

220
210

220
Down-_Dryer Con
: Failure
SOp Removal
Efficiency
c/
/>->


77.2

77.8

77.8
76.1
76.5

75.6
75.3

75.0
2100
183
100
                                                                  > 500   Blow back from
                                                                          stack gas back
                                                                          pressure

-------
                    BOILCR/SCRliBRER DATA DUKlXt',  TRANSTCNT CONIU'TIONS


1
w
K)
1
r>-4-~ 1
LJ IA •- V- '
Time
1120
1140
1200
1220
1240
1300
1400
r\ op otWK ovt "7 It
±J> X— i— -W^IWV -—A. « .
Boiler
Load
(M\v)

179
179
179
o>_._^ .-._„ ii?n-i
i J.IHV, op<-ll 1
Scrubber £> P
2nd Stage
(in. H?0)

3.0
5.0
7.5
400 T>>-.nT\o ; fin t- Cf\r>r)
Scrubber
Inlet Scrubber
ACFM pn
135,700
140,800 7.5
146,400 7.4
173,100 7.3
i t T nn Sen
Inlet
S02
(ppm)
800
750
780
875
ubber First
UO-1250)
Outlet
S02
(ppm)
200
270
220
120
Stage Outage
SO p Removal
Efficiency
o.;
75.0
64.0
71.8
86.3
THR*

83.15

*THR = Theoretical Removal Efficiency calculated from Ghemico  Efficiency Equation.

-------
                    BOILER/SCRUBBER DATA DURING TRANSIENT CONDITIONS
Date 7 December 74 Time Span 1630-1900 Transient Condition Scrubber Start Up










i
H
I-1
U)
1






Boiler
Load
Time (MW)
Start Up
1630
1640
1650
1700 165
1710
1720
1730
1740
1750
1800 167
1810
1820
1830
1840
1850
Scrubber A. P Scrubber Inlet
2nd Stage Inlet Scrubber S02
(in. H20) ACFM pH fppm)


900

0.8 188,400 7.1 900

900

860

0.8 188,400 7.1 950

930

930

Outlet
S02
(ppm)



270

210

210

205

210

205

205
SOp Removal
Efficiency
/b



70.0%

76.7

76.7

76.1

77.9

78.0

78.0
1900
173
2.8
                                   188,400
7.2
940

-------
BOlLllR/SCRilBRCK DATA DI'KiVO  TRANS]IINT CONDITIONS
Date 8 December 74 Time Suari 0600-2400 Trwrm


Time
0600
0700
0800
0900
1000
, 1100
w
£ 120°
1 1300
1400
1500
1600
1700
1800
1900
2000
2100
2200
2300
2400
Boiler
Load
(MW)
180
179
177
146
144
143

137
127
110
110
106
102
103
96
97
102
102
100
102
Scrubber A. P
2nd Stage
(in. H?0)
8.5
8.5
8.5
8.3
8.1
8.1

7.3
6.0
6.2
3.5
3.5
. 3.8
5.6
3.8
3.9
3.9
3.5
3.8
4.0
Scrubber
Inlet
ACFM
183,400
188,400
183,400
183,400
180,200
100,200

173,100
165,900
165,900
146,400
146,400
153,600
153,600
180,200
183,400
138,400
183,400
138,400
138,400
;it>nt- r i-i n Hi firm DroDoins Load

Sorubber
PH
7.0
6.9
6.8
6.7
6.9
6.9

6.9
6.9
6.9
6.9
7.2
7.0
7,0
7.0
7.1
7.1
7.2
7.2
7.0
Inlet
S02
(ppm)
1000
950
1000
1200
1100
1200

1100
1200
1100
1100
1050
1050
1020
1020
1020
1100
1000
1050
1100
Outlet
S02
(ppm)
135
140
180
200
200
200

220
240
220
240
250
250
260
260
270
280
240
280
290
Because nf WP
SO 2 Removal
Efficiency
%
86.5
85.3
82.0
83.3
81.8
83.3

80.0
80.0
80.0
78.2
76.2
76.2
74.5
74.5
81.4
74.5
76.0
73.3
73.6

-------
                               BOILKR/SCRUBBER DATA DUR.INC TRANSIENT CONDITIONS
 I
o
M
cn
e 9 December 74 Time Span 0700-1200 Transient Condition Rising Boiler Load

Time
0700
0800
0900
1000
1100
1200
Boiler
Load
(MW)
100
99
161
185
185
185
Scrubber A P
2nd Stage
(in. H?0)
4.4
4.3
4.5
4.5
4.3
4.7
Scrubber
Inlet
ACFM
188,400
108,400
197,600
197,600
197,600
218,100

Scrubber
Pli
7.1
7.1
7.1
7.0
6.9
6.9
Inlet
S02
(ppml
1200
1050
1100
900
850
850
Outlet
S02
(ppm)
320
220
230
220
185
175
SOp Removal
Efficiency
/*w
73.3
79.0
79.1
75.5
78.2
79.4

-------
                                BGILCR/SCRUBnER DATA Dl'RINC  TRANSIENT CONDITIONS
Date 11 December 74 Time Span 04-00-0500 Transient Condition Scrubber Shut Down- Leak in Bleed
Line
Boiler Scrubber A P Scrubber Inlet Outlet SO-, Removal
Time
0400
0425
0500
Load 2nd Stage
fMW) fin. H?0)
163 1.0
Scrubber Down
163 0.0
Inlet Scrubber S02 S(>2 Efficiency
ACFM pH fppml fppm) %
180,200 7.2 1100 240 78.2
100,200 7.1 1100 ^>1000 Back flow due to
                                                                                      stack gas back
                                                                                      pressure
i
M

-------
BOUXR/SCRWBr.R DATA DURJNil  TRANSIENT CONDITIONS
Date 13 December 74Time Span 1810-2200 Transient Condition Scrubber Start Up


Time
1810
1855
1900
1910
1920
2000
2100
2200
w
Bniler
Load
(MW)
120

118


111
116
113

Scrubber ^ P
2nd Stage
fin. H?6)
1.4

3.2


2.7
2.7
5.3

Scrubber
Inlet
ACFM
223,400

228,400


242,200
228,400
242,200


Scrubber
PH
7.2

7.2


7.1
7.1
6.8

Inlet
SO 2
fPPm)
1250


1150

1180
1200
1250

Outlet
S02
fPPm)

240


285
290
275
235

SOp Removal
Efficiency
%

80.8%
77.2

75.2
75.4
77.0
81.2


-------
I
W
                                  B()HJ':i
-------
                                 BOILKR/SCRUBBER DATA DI'RINC  TRANSICNT CONDITIONS
i
n
M
vo
I
e 16 December 74Time Span 1300-1700 Transient Condition Scrubber 2nd stage down & start



Time
1200
1300
1310
1322
1343
1352
1400
1412
1424
1439
1457
1500
1510
1515

1520
1530
1S40
1550
1555

Boiler
Load
(MW)
146
146




146




143
Scrubber
135

135
110
78
110
165

Scrubber A P Scrubber
2nd Stage Inlet Scrubber
fin. H?0) ACFM Di[
6.4 159,700
0.0 7.5




0.0 74,800 > 8




0.0 82,900 >8
Start Up (2nd Stage)
(1.0)
Assumed




1.8 7.5
up;
Inlet
SU2
(ppm)
940


890

885


890

900
900




600
450


wet coal
Outlet
S02
(ppm)
160

685

685


680

790


135
115

115

100
110
80

SOo Removal 02
Efficiency %
% In Out
83.0



23.0


23.6

20.0


85.0
87.2

87.2
10.0+
77.8 10.*
75.6 9.0
82.2 10. +

-------
I
M

BOILP.R/SCRli
BBER DATA DL'RJXC TRANSIENT CONDITIONS
Date 17 December 7 4Time Span 0900-1400 Transient Condition Experiements changing the
Boiler
Load
Time (MW)
0900 151
0950
1000 162
1035
1100 174
1130
1150
1200 182
1225
1245
1300 182
1320
1400 182
Scrubber A
2nd Stage
fin. H?0)
3.7
8.2
8.2
8.0
8.7
7.4
6.2
6.0
6.6
8.3
8.5
9.5
9.7
P Scrubber
Inlet Scrubber
ACFM pi!
130,600 7.2
7.1
159,700 7.1
7.0
159,700 7.0
7.0
7.0
180,200 7.1
7.2
7.3
197,600 7.1
180,200 7.2
liquid
f 1 ow rat*3 in the scrubber 2nd stags
Inlet Outlet SO-, Removal Liquid
S02 S02 Efficiency Flow
(ppm) (ppm) % Rate*
790
1050
1050
1020
950
900
850
960
880
810
810
805
790
165
170
170
135
135
170
195
180
180
120
135
110
110
79.1
83.8
83.8
86.8
.85.8
81.1
77.1
81.3
79.5
85.2
83.3
86.3
86.1
5900
7000
6800
5100
4000
5100
5000
5800
5800
            *Liquid Flow Rate (MgO)  (gpm)

-------
                              BOILER/SCRUBBER DATA HURINC TRANSIENT CONDITIONS
I
w
Date 19 December 74Time Span 0800-1300 Transient Condition Scrubber Second
Time
0800
0900
1000
1100
1200
1300
Boiler Scrubber A
Load 2nd Stage
(MW) (in. H?6)
157 8.5
157 8.4
157
156
-
Scrubber completely
P Scrubber
Inlet Scrubber
ACFM p]|
197,600 7.0
207,400 7.0
159,700
165,900
165,900
shut down.
repair
Inlet
SO 2
*1200
1200
1200
1200
1200

2nd stage
Outlet
(ppm)
234
230
>300
>300
>300

Stage Outage to
recycle header
S02 Removal
Efficiency
o/
/P
80.5
80.8
<75.0
< 75.0
<75.0

           *Readings from DuPorit Analyzer

-------
I
w
to
to
I
                               BOILER/SCRUBBER DATA DURJNC TRANSIENT  CONDITIONS
Ic 13 D eu'eaniJtiJf ?H '!'
Time
Start Up
1600
1700
1800
Boiler
Load
CMW)

-
150
143


ime Span J.DUU-J.OUU Trans
Scrubber £» P
2nd Stage
fin. H?0)

2.8
6.0
6.2
Scrubber
Inlet
ACFM

173,100
133,400
197,600
lent Condition Scrubber Start Up
Scrubber
pH

7.0
7.1
7.1
Inlet
SO 2
(PPn-Q
1200
1300
1200
Outlet
St>2
(ppm)

>300
220
228
SOp Removal
Efficiency


-------
                                 BOILER/SCRUBBER DATA Dl-RJN'C TRANSIENT  CONDITIONS
 I
n

OJ
 i
e 20 December 74 Time Span 0700-1200 Transient Condition Wet Coal-Boiler Feed Problem
Time
0700
0800
0900
1000
1100
1200
Boiler
Load
(MW)
90
99
98
94
88
90
Scrubber A P
2nd Stage
(in. H?0)
3.5
3.4
3.6
3.6
3.6
3.8
Scrubber
Inlet
ACFM
99,300
91,100
99,300
—
—
__
Scrubber
Pll
7.0
7.0
7.0
7.0
7.0
7.2
Inlet
SO 2
1180
1200
1180
1180
1020
960
Outlet
(ppm)
280
285
240
240
200
186
SOp Removal
Efficiency
76.3
76.3
79.7
79.7
80.4
80.6

-------
I
n
                              BOILER/SCRUBBER DATA DURIN'C TRANSIENT CONDITIONS
C C.L. Ecv; efiilitM' 74- 1'
Time
0800
0900
?. oiler
Load
(MW)
136
140
irne Span ueuu-lluu Transient Condition Scrubber Shut
Scrubber <£. P
2nd Stage
fin. H?6)
6.2
^
Scrubber.
Inlet
ACFM
135,700
—
oc- rubber
PH
7.1
_
Inlet
SO 2
fPPni)
980

Outlet
SC)2
fppm)
180

Down-Leaks Star
SO P Removal
Efficiency
?'o
81.6

Start Up


1000       166


1100       174
                                 6.2
200
7.2
890
128
85.6

-------
BOILCR/SCRUBBER DATA DURJNO TR/\NSTCNT CONDITIONS




1
H
to
l/i
1
Date .22 December 74 Time Span 0800-1100 Transient Condition Scrubber Start Up
Boiler Scrubber A p Scrubber. Inlet Outlet SOp Removal
Load 2nd Stage Inlet Scrubber SO^ S02 Efficiency
Time (MW) (in. H20) ACFM pH fppm) (pptrO %
1020 166
1100 174 6.2 140,800 7.2 890 128 85.6
1200 173 6.2 140,000 7.2 800 140 82.5
1300 174 6.3 140,800 7.1 800 200 75.0


-------
 I
M
fo
                                                DATA DIT-iINC TRANSIENT CONDITIONS
Date 23 December 74 Time Span 0800-0900 Transient Condition Scrubber Shut Down-Leaks in first
Time
0800
0900
0930
Boiler
Load
CMW)
140
169
Scrubber ^ P
2nd Stage
fin. HpO}
8.0
6.2
Scrubber
Inlet
ACFM
173,100
146,400
Scrubber
PH
7.0
7.2
and
Inlet
S02
880
860
second stage.
Outlet SO
S02 Ef:
fppm)
160
160
P Removal
ficiency
81.8
81.4

-------
                   BOILCR/SCRUBBER DATA DURilNC TRANSIENT CONDITIONS
Date 29 December 7 i* Time Span 1600-1800 Transient Condition Scrubber Shut Down-Leak in elbow
of 1st stage
Time
1600
1700
Boiler
Load
fMW)
137
-
Scrubber A P
2nd Stage
fin. H?0)
3.5
0.0
Scrubber.
Inlet
ACFM
165,900
130,600
So rubber
PH
7.1
7.7
Inlet
SO 2
fPP"0
1680
200
Outlet
S()2
fPPm)
300
1600
SOp Removal
Efficiency
%
82.1
Back flow froi
                                                                              stack gas
                                                                              pressure
1800
130,600

-------
i
M
K>
00
I
                             BOILER/SCRUBBER DATA DUR.lK'i; TRANSIENT CONDITIONS
e S January ,/b
Time
1400
1500
1600
Boiler
Load
(MW)
181
DOWN
Shut Down - Leaks in 1st Stage
'ime Span 1400-1700 Transient Condition Start Up - 1st Stage only
Scrubber -4- P
2nd Stage
fin. H?0)
-
FOR REPAIRS
Scrubber.
Inlet
ACF«~
120,300

Inlet
Scrubber S02
pH fppm)
8 1380

Outlet
S02
fppm)
1290

SO 2 Removal
Efficiency
0 '
/!••
6.5%

         1700
176
1.0
1300
1220
6.2%

-------
BOILER/SCRUBBER DATA DURINC TRANSIENT CONDITIONS
Date 8 January 75 Time Span 1700-2400 Transient Condition Scrubber operating with only ]




i
w
ro
vo
I

Time
1700
1800
1900
2000
2100
2200
2300
2400
Boiler
Load
fMW)
176
179
179
181
180
183
Scrubber ^ P
2nd Stage
fin. H?0)
1.0
3.4
4.0
4.0
4.0
4.0
4.0
4.0
Scrubber.
Inlet
ACFM
180,200
255,000
291,800
291,800
291,800
291,800
291,800
438,300
Inlet
Sorubber S02
pH fppm)
8 1300
1320
1300
1380
1390
1390
1430
" 1430
Outlet
S02
fppm)
1220
1290
1290
1340
1260
1280
1340
1340
Ste
S02 Removal
Efficiency
o/
6.2
2.3
0.8
3.5
9.4
7.9
6.3
6.3
                                              AVERAGE:
5.3

-------
i
w
o
I
                              BOILRR/SCRURBER DATA DURJNC. TRANSIENT  CONDITIONS
                        C    ~

Time
0800
0830
-——- j , — A JL.1I
Boiler
Load
cm)
119
SHUT DOWN
I»V- «_I|J>C%AI 	 •*-*
Scrubber A P
2nd Stage
fin. H?0)
-

wv — ** L JL all r:
Scrubber
Inlet
ACFM
266,200

>j.t:ii L cuuu.
Scrubber
PH
-

          r>i         —                      -   '
Condition o*mt: Duwn-ntipairs & ^reparation istj

                                 Stage Only

       Inlet    Outlet     SOp  Removal

        S02      S02       Efficiency

       CPPm)     (ppm)         %	
                                                                    900
                 800
11.1

-------
                                BOTU'.R/SCRUBBER DATA Dl'RINC  TRAMS] CNT
I
n

e 18


Time
1304
1355
1410
1425
1440
1505
1520
1530
1545
1600
1615
1630
1645
1700
1730

January 75
Boiler
Load
(MW)


126


150



178




SHUT
Start
Time Span 1340-1730 Transient Condition (1315)
Up- Shut
Screw
Scrubber A P Scrubber Inlet Outlet
2nd Stage Inlet Scrubber 862
(in. H?0) ACFM pH fppm)
860

5.6 197,600 7.5 810

940
4.2 188,400 7.2
900

860
5.4 188,400 7.3 900

900

850
DOWN
S()2
(ppm)

200

140

180

170


140

120


Down (1730)
Conveyer Overloa
SOp Removal
Efficiency
•:/

76.7

82.7

80.9

81.1


84.4

86.7



-------
BOILER/SCRUBBER DATA DURlMfl TRANSIENT CONDITIONS
Dsite_ 19 Jar)uaz°y 75 Time Span 1130-1345 Transput- r-^r.^



H
CJ
to
i

Time
1130
1145
1200
1215
1230
1245
1300
1315
1330
1345
Boiler Scrubber £ P Scrubber
Load 2nd Stage Inlet Scrubber
(MW) fin. H?0) ACFM pH

177 3.4 180,200 7.5
175 4.4 173,100 7.2
SHUT DOWN
Start Up - Shut Down
:ior. (1130) (1345 1«L Stage Qve
Inlet
S02
1100
1050
1000
1000
Outlet
S02
fppm)
200
190
195
200
180
SOp Removal
Efficiency

82.7
81.4
80.0
82.0

-------
                    BOILER/SCRUBBER  DATA DURJNC, TRANSIENT CONDITIONS
Date 23 January 75 Time Span 1445-1700 Transient Condition Start Up









i
w
OJ
OJ


Time
1445
1500
1515
1535
1550
1605
1620
1635
1650
Boiler Scrubber <£ P
Load 2nd Stage
(Mlv) fin. H?0)
START UP
181 1.8



178 2.0



Scrubber Inlet
Inlet Scrubber S02
ACFM pll fppni)

78,800 7.7 1180

- 1200

74,000 7.6 1250

1190

Outlet
SO 2
fppm)


100

280

290

270
SOp Removal
Efficiency
%


91.5

76.7

76.8

77.3
1700
176
3.2
120,300
6.9
1180

-------
BOILER/SCRUBBER DATA DURJN(i TRANSIENT CONDITIONS
Date 27 January 75
Boiler
Load
Time (MW)
0520
0530
0545
0600 115
0615
0630
0645
0700 163
0715
i 0730
2 0745
* 0800 176
0815
0830
0845
0900 162
0915 •'
0930
0945
1000 116
1015
1030
1045
1100 138
1115
1130
1145
Time Span 0600-1540 Transient Condition Start
Scrubber A P Scrubber Inlet
2nd Stage Inlet Scrubber S02
fin. H?0) ACFM pH fppm)

1100

0.7 ~ 7.4 1100

1000

1.8 -- 7.4 1000

1000

0.2 — 7.5 900
880

856
13.0 309,200 7.5
900


10.8 255,000 7.4 900

900

10.2 242,200 7.2 900

1000

Up- High
Outlet
S02
fppm)


230

240

250

250

220


170

80

63
50

75

90

110

120
Gas Flow- Shut
SOp Removal
Efficiency
%


79.1

78.2

75.0

75.0

78.0


80.7

90.6

93.0
94.4

91.7

90.0

87.8

88.0

-------
BOILER/SCRUBBER DATA Dl.IR.JNC TRANSIENT CONDITIONS

Date 27 January
75
Boiler



i
n
u>
Ul


Time
1200
1220
1235
1250
1305
1320
1345
1400
1415
1430
1445
1500
1510
1520
Load
(MW)
174

175
174
173

Time Span Continued Trarisien
Scrubber ^ P
2nd Stage
(in. H?0)
8.0

7.8
8.0
2.2

Scrubber
inlet Sc
ACFM
207,400

207,400
228,400
188,400

t Condition Start
Inlet
rubber SO 2
pll (ppni)
7.2 1000
1000

7.3 1000
1000
7.1
1000
1000
7.2
950

Up-High
Outlet
S()2
Cppm)
120
120
130
120
115
200
205
Gas Flow- Shut
SOp Removal
Efficiency
88.0
88.0
87.0
88.0
88.5
80.0
78.4

-------
                          BOILER/SCRUBBER DATA DURING TRANSIENT CONDITIONS



1
w
OJ
Date
Time
1435
1800
2000
2200
11 August 75 Time
Boiler
Load
(raw)
185
182
183
183
Scrubber /\ P
Second Stage
(in.HoO)

2.6
3.4
3.4
Span 1435-2200
Scrubber
Inlet
ACFM
87,000
218,100
218,100
218,100
Scrubber
pH

7.7
7.3
7.1
Transient Condition Start up
* Inlet
S02
(ppm)
900
900
900
*Outlet
so2
(ppm)

264
264
264
S02 Removal
Efficiency

70.7
70.7
70.7
Velocity
FPM




*DuPont Unit

-------
w
u»
                              BOILER/SCRUBBER DATA DURING TRANSIENT CONDITIONS
     Date  15 August 75
_Time  Span 0200-0400
           Boiler   Scrubber A P   Scrubber
            Load    Second Stage    Inlet     Scrubber   S02
     Time   (mw)      (in.HoO)      ACFM         pH     (ppm)
       _Transient Condition Complete Shut Down/
                            Dryer plugged
       Inlet   Outlet   S02 Removal
     0200     178        3.8
     0400     Shut Down
      188,400
7.2
*1080
 so2
(ppm)

*240
                                              Efficiency
77.8
                                      Velocity
                                        PPM
     *DuPont Unit

-------
                         BOILER/SCRUBBER DATA DURING TRANSIENT CONDITIONS
Date    22 August  75	Time Span    1400-1600
Transient Condition
         0.1 iu
ity increase










1
n
w
00
1











Boiler Scrubber A P Scrubber
Load Second Stage Inlet
Time (mw) (in.H.,0) ACFM
1400 176
1430 Start
1438
1439
1440
1441
1442
1443
1444
1445
1446
1447
1448
1449
1450
1500 153,600
1515
1530
1600 177 2.0 165/SOO

Inlet
Scrubber S02
pH (ppm)
20
20







1000
1020
1050
1100
1100
1100



7.4 1190

Outlet
so2
(ppm)
1000
1050
1070
1070
1070
800
500
200
250
300





370
380
380
360
(1620 FPM
S02 Removal
Efficiency
%





_



70.0





69
68
68
68
to 2025 FPM)

Velocity
FPM
930
1175
1500
1500
1560
1430
1375
1375
1375
1375
1430
1500
1500
1500
1500
1560
1560
1560
1620

-------
                               BOILER/SCRUBBER DATA DURING TRANSIENT CONDITIONS
I
M
OJ

Date


Time
1600
1630
1645
1700
1715
1730
1745
1800


22 August 75 Time
Boiler
Load
(raw)

177

179



184
Scrubber A P
Second Stage
(in.HoO)
2.0



,


3.2



Velocity
increase
Span 1630-1800 Transient Condition (1620 FPM to 2025 FP»
Scrubber
Inlet
ACFM
165,900


173,100



207,400
Inlet
Scrubber S02
pH (ppm)

1200
1200
1190
1130
1130
1150
7.3 1170
Outlet
so2
(ppm)

370
370
330
330
310
300
300
S02 Removal
Efficiency
%

69
69
72.3
70.8
72.6
74
74.4

Velocity
FPM

1620
1560
1760
1940
2025
1940
1940

-------
                              BOILER/SCRUBBER DATA  DURING TRANSIENT CONDITIONS
     Date   23 August 75
_Tirae  Span   2100
Transient Condition  Centrifuge Clog/
I
w

o
I


Time
2000
2100
2115
2120
2125
2200
2300
2315
2330
2345
2400
2415
2430
0100
0200
0300
0303
0304
0305
0309
Boiler Scrubber ^ P Scrubber
Load Second Stage Inlet
(mw) (in.HoO) ACFM
174 3.2 207,400
180



178 1.5 146,400
174 146,400



158 120,300


114
107
104



Scrubber off
Inlet Outlet
Scrubber S02 S02
pH (ppm) (ppm)
7.0 *1500 *360
400
400
400
500
7.0 *1080 *480
480
480
450
470
500
550
500
480
480
420
420
420
420
1000
Complete Shut Down
S02 Removal Hastings
Efficiency Voltage/
%
76.0
73.3
73.3
73.3
66.7
55.6
55.6
55. -6
58.3
56.5
53.7
49.1
53.7
55.6
55.6
61.1
61.1
61.1
61.1

Velocity
3.3V/2025
3.3v/2025
3.3v/2025
2.4V/1375
2.4V/1375
2.5V/143Q
2 . 4V/1375
1.7v/1025
1.9v/1125
2.1v/12i5
2.1v/1225
2.3v/1325
2.0V/1175
1.9V/1125
2.0V/1175
2.0V/1175
2.0V/1175
1.6V/1025
1.2V/810

     *DuPont  Unit

-------
                          BOILER/SCRUBBER DATA DURING TRANSIENT  CONDITIONS



1
w
•u
I-
1
Date
Time
1300
1330
1400
1500
1600
25 August 75 Time
Boiler Scrubber &P
Load Second Stage
(mw) (in.H->0)
184
Start Up
175 1.8
178
182 3.5
Span 1300-1600
Scrubber
Inlet Scrubber
ACFM pH


173,100 7'3
173,100
180,200 7.3
Transient Condition Start Up
Inlet
S02
(ppm)

1080*

1140*
Outlet S02 Removal
S02 Efficiency
(ppm) %


360* 66.7

300* 73.7
Velocity
FPM





*DuPont Unit

-------
BOILER/SCRUBBER DATA  DURING TRANSIENT CONDITIONS
Date


Time
0400
0415
0500
0515
0600
0700
0710
0715
, 0716
w 0717
*» 0718
0719
0720
0730
0800
0815
0900
1000
1030
1045
1100
1200
1230
1245
1300
1330
1345
1400
26 August 75 Time Span 0400-1400 Transient Condition Rapid v<
Boiler
Load
(raw)
176

183

180
176








177

176
178


180
184


185


185
Scrubber A P Scrubber
Second Stage Inlet
(in.HoO) ACFM
3-2 197,600



3.4 197,600
125,400








0-9 125,400

120,300
0.8 120,300


146,400
1.6 146,400


173,100


3.6 197,600
Inlet
Scrubber S02
pH (ppm)
6.9 1300
1200
1200
1380
6.9 1320
1350

1300
1200
1150
1370
1350
1300

7.2 1340
1340
1350
7.1 1340
1290
1290
1250
7.1 1250
1250
1200
1200
1120
1100
6.8 1100
Outlet
so2
(ppm)
390
400
420
470
400
470
470






470
. 540
540
490
450
420
420
410
420
420
370
350
320
300
300
SO 2 Removal
Efficiency
%
70.0
66.7
65.0
65.9
69.7
65.2
65.2






63.9
59.7
59.7
63.7
66.4
67.4
67.4
67.2
66.4
66.4
69.2
70.8
71.4
72.7
72.7
                                                           Velocity
                                                             FPM
                                                             1840
                                                             1175
                                                             1275
                                                             1560
                                                             1940
                                                             1225
                                                             1275
                                                             1175
                                                             1275
                                                             1275
                                                             1275
                                                             1225
                                                             1275
                                                             1225
                                                             1225
                                                             1275
                                                             1175
                                                             1175
                                                             1175
                                                             1430
                                                             1375
                                                             1430
                                                             1430
                                                             1690
                                                             1690
                                                             1940
                                                             1940
                                                             1940

-------
                               BOILER/SCRUBBER DATA DURING TRANSIENT CONDITIONS
i
W
Date 26 August 75 Time Span 1850-1920 Transient Condition 2nd stac
Boiler Scrubber £. P Scrubber
Load Second Stage Inlet
Time (mw) (in.H00) ACFM
1800 178 3.5
1830 Shut Down
1845
1850
1855
1900 174 173,100
1905
1910
1915
1920
Inlet
Scrubber S02
pH (ppm)
7.1 1175
1175
1140
1140


1120
1120


Outlet
so2
(ppm)
350
330
320
320
400
900


1000
1000
S02 Removal
Efficiency
%
70.2
71.9
71.9
71.9
64.9
21.1


10.7
10.7
Velocity
  FPM

  1500
  1500
  1500
  1500
  1620
  1690
  1690
  1620
  1690
  1690

-------
                                BOILER/SCRUBBER DATA DURING TRANSIENT CONDITIONS
I
W
Date
Time
1400
1415
1430
1445
1500
1515
1530
1535
1536
1537
1538
1539
1540
27 August 75 Timc Soan 1400-1540
Boiler Scrubber A P Scrubber
Load Second Stage Inlet Scrubber
(raw) (in.HoO) ACFM pH
175 87,000


180 87,000
Shut Down






Tv-ai-ioT •
Inlet
S02
(ppm)
1390
1350
1350
1200
1275
1275
1080







Outlet
so2
(ppm)
1200
1200
1140
1150
1150
1100

900
900
900
900
1000
1025
i4.j — let- S+*q'
S02 Removal
Efficiency
13.7
11.1
15.6
4.2
9.8
13.7








Hastings
Voltage/
Velocity^
1.3v/350
1.3v/850
1.3v/850
1.2v/810
1.3v/850
1.3V/850
1.3v/850
1.2V/810
l.lv/770
l.Ov/730
0
0
0
      Average
11.4

-------
                  APPENDIX F




LISTS OF SCRUBBER MALFUNCTIONS AND MAINTENANCE
                       -Fl-

-------
-F2-

-------
       LIST OP




SCRUBBER MALFUNCTIONS
         -F3-

-------
 Date

Oct. 8
Oct. 8
Oct. 9

Oct. 9

Oct. 9
Oct. 9

Oct. 9
Oct. 10
Oct. 10

Oct. 11
Oct. 12

Oct. 12


Oct. 14

Oct. 14
Oct. 14
                Type of
              Malfunction
           Centrifuge hopper clogged
           "A" first stage recycle
           pump won ' t start
           Leak in second  stage
           suction header
           Centrifuge chute clogged
           "A" MgO pump not operat-
           ing properly
           MgS03 weigh belt out of
           order
                                     Shut-down
                                     Required

                                         Yes
                                         No
                                         No

                                         No
                                         No

                                         No

                                         No
           ID fan kicked  out             Yes
           Centrifuge hopper clogged      No

           Bucket elevator ball  bearings
           failed                        No
           "B" recycle pump  and. line
           clogged                       No
           Leak in suction header of
           "C" recycle pump               No

           Leak in seal of "B"  MgO
           pump                          No
           Centrifuge hopper clogged      No
           Leak in first stage  discharge
           line at elbow                 Yes
Duration
of Outage

j nr.
                                                1 hr.
                                                27 hrs.
Oct.  15    Centrifuge seized
                                         No
        Remedial Action Taken

Blank installed ahead of leak
Diverted centrifuge; wash hopper and
dryer with water
          Breaker repaired

          Repaired, on Oct. 10
          Divert centrifuge; wash chute

          Pump replaced during  shutdown

          Bypass used

          Restart fan
          Divert centrifuge; wash hopper
                                                          Divert centrifuge; lower fan amps;
                                                          replace bearings

                                                          Lower fan amps; wash out pump and
                                                          line
                                                          Switch to "B" pump; leak sealed itself
                                                          on "C" pump
                                                          Repaired during Oct. 18 outage
                                                          Divert centrifuge; wash hopper          i

                                                          Inspect and replace line with a blank

                                                          Bump the start switch and it broke loosi

-------
tn
I
                                                       *5 days
                                                       6% hrs.
                Type of              Shut-down  Duration
 Date         Malfunction            Required   of Outage

Oct. 16    South pinch valve leaking     No

Oct. 18    l.Leak in 6" blank at top
             of scrubber
           2.Leak in gasket of 14"       Yes
             first stage blank
           3.6" pinch valve liner
             leaking
           4. "A" and "B" transfer
             pumps leaking

Oct. 22    "A" dilution tank agitator
           not working                   No
Oct. 23    Leak in pH meter pot          No
Oct. 23    Two leaks in centrifuge
           case                          No
Oct. 23    Leak in "B" recycle pump      No

Oct. 24    Leak in discharge line from
           sump pump                     No
Oct. 24    Centrifuge chute clogged      No
Oct. 24    Discharge line on "A" MgO
           pump clogged                  No

Oct. 25    Centrifuge hopper clogging
           continuously                  No
Oct. 25    Boiler tube leaks             Yes
                                                                        Remedial Action  Taken
                                                       15 days
                                                       21 hrs.
      Nov. 10    pH meter not working          No
      Nov. 10    Leak in centrifuge cover      Yes
                                              (Nov.11)
                                                                 Leak plugged
*Repairs 1 through 4 took 2 hrs.  45 mins.
At start up, leaks developed in the MgO
magnetic flow meter to the tangential
sprays
"B" tank used; oil replaced in "A"
tank gear box

Leak plugged
One leak plugged; the other couldn't
be reached
"C" pump put in service; re-wrap "B" pump
Repaired Nov. 7
Bypass centrifuge; unplug chute

Switch to "B" pump; clean "A" pump

Divert centrifuge; wash hopper, adjust
vibrator cycle time

Repaired

Readings taken on bench pH meter
Repaired during next outage

-------
                Type of              Shut-down  Duration
 Date         Malfunction            Required   of Outage

Nov. 10    Steam control valve not
           operating properly            No
Nov.10     Leak in mother liquor
           return line                   No

Nov. 11    1.Large leak in second
             stage bleed line            Yes     2 days
           2.Leak in pH meter                   18 hrs.
           3.Leak in bypass around
             second stage recycle
             pump discharge, valve

Nov. 13    pH meter inaccurate           No
Nov. 14    Leak in centrifuge cover      No
Nov. 14    Centrifuge hopper clogged      No
Nov. 14    "B" thickener valve opened
           up causing the dilution tank
           to overflow                   No
Nov. 14    MgO weigher motor not
           operating                     No

Nov. IS    Leak in centrifuge cover
           gasket                        No
Nov. IS    Leak in "B" thickener         No

Nov. 16    "A" second, stage recycle
           pump noisy and vibrating      No
Nov. 16    MgS03 conveyor kicked out
           twice                         No
Nov. 16    Centrifuge hopper clogged      No
Nov. 16    MgSC>3 weigh belt broke        No
        Remedial Action Taken


Operate valve manually

Repaired during next outage


Repaired
Readings taken on bench pH meter.
Meter repaired on Nov. IS

Repaired Nov. IS
Divert centrifuge; wash hopper
Valve reset

Electrician called to repair
Repaired Nov. 18
"A" thickener put into service

Switched to "B" pump until "A" is
inspected

Divert centrifuge; clean out restriction
Divert centrifuge; wash hopper
Placed on bypass until repaired

-------
-vl
I
 Date

Nov. 16

Nov. 16



Nov. 19

Nov. 20

Nov. 20
Nov. 20

Nov. 21
Nov. 21
Nov. 21

Nov. 21
Nov. 21
       Nov. 24


       Nov. 25

       Nov. 25

       Nov. 26

       Nov. 26
                       Type of               Shut-down
                     Malfunction             Required

                  MgSC>3 bucket elevator
                  kicked out three times        No
                  6" pinch valve liner in
                  the first stage recycle
                  line ruptured                 Yes

                  Leak in centrifuge cover      No

                  Inside bearing on dryer
                  conveyor broke                No
                  Centrifuge hopper clogged     No
                  New leak in centrifuge cover  No
                                     Duration
                                     of Outage
                  Bucket elevator tripped
                              No
Rappers on the dryer fell off No
Thermocouple and conduit on
dryer broken off              No
Centrifuge hopper clogged     No
Belts on dryer ID fan burnt   Yes
off
           Dryer screw conveyor hub
           failure                       Yes

           MgSC>3 solid equipment kick
           out                           No
           Centrifuge cover leaks        No

           Centrifuge hopper clogged.
           twice                         No
           Hole in 6" recycle water
           line on first stage           No
                                      2 days
                                      20 hrs.
                                                        2 days
                                                        7 hrs.
        Remedial Action Taken


Divert centrifuge; dig out buckets


Repaired during shutdown

Welded on Nov. 22
Repaired Nov. 22
Divert centrifuge; wash hopper
Welded on Nov. 22

Dig out boot
Replaced Nov. 22

Repaired Nov. 22
Divert centrifuge; wash hopper
Belts replaced in 2% hours.  The
dryer ID fan would not start.  During
this outage the boiler burst a tube
causing Unit #3 to go off line.
                                         hrs.    Hub replaced
                                                Dig out buckets  and  dryer screw conveyor
                                                Welded  during outage
                                                Divert  centrifuge;  wash hopper

                                                Temporary  rubber  patch applied

-------
00
I
                Type of              Shut-down  Duration
 Date         Malfunction            Required   of Outage

Nov. 21    First stage level con-
           troller and MgO level
           controller not working         No
Nov. 27    Centrifuge hopper clogged      No

Nov. 28    Leak in first stage distrib-
           ution header                  No
Nov. 28    Dryer clogged                 No

Nov. 28    Drain nippel in sump
           pump leaking                  No
Nov. 28    pH meter out of calibration    No

Nov. 29    Leak in 6" bleed line from
           first stage                   No
Nov. 29    Dryer clogged                 No

Nov. 30    Centrifuge hopper clogged      No
Nov. 30    Leak in 6" bleed line worse    No

Dec. 1     Southwest torus spray
           broke off                     No
Dec. 1     Leaks in 6" bleed line  out            3  days
           of control                    Yes      18 hrs.

Dec. 5     Leak in first stage discharge
           header   .                     No

Dec. 7     Leak in 6" first stage  re-
           cycle line at pinch valve      No
Dec. 7     Centrifuge hopper clogged      No

Dec. 8     MgO weigh feeder belt ran
           off track                     No
                                                                          Remedial  Action  Taken
                                                                  Repaired
                                                                  Divert centrifuge;  wash hopper
                                                                  Hole patched  temporarily
                                                                  Centrifuge diverted;  dryer allowed  to
                                                                  clean itself
                                                                  Recalibrate
Pipe clamps installed
Divert centrifuge; allow dryer to clear

Divert centrifuge; wash hopper
Pipe clamps installed

Flows cut back to torus sprays; un-
successful attempt to install blind

Temporary replacement line installed
                                                                  Stop recycle;  install blind
                                                                  Patch leak
                                                                  Divert centrifuge;  wash  hopper
                                                                  Reset belt

-------
                        Type of              Shut-down
         Date         Malfunction            Required

        Dec. 8     New leak in 6" first
                   stage recycle line           No
        Dec. 8     Centrifuge hopper clogged     No
        Dec. 8  .   Dryer clogged                No
                                                Duration
                                                of Outage
Remedial Action Taken
                                                          Patch hole
                                                          Divert centrifuge; wash hopper
                                                          Divert centrifuge; allow dryer to
                                                          clear itself
VO
i
Dec. 9     Transition pipe at screw
           feeds clogged                No

Dec. 10    Centrifuge hopper clogged     No
Dec. 10    Centrifuge cover leak        No

Dec. 11    Leaks in 6" first stage
           bleed line                   Yes

Dec. 12    6" first stage bleed line
           sleeve failure               Yes

Dec. 13    Mother liquor agitator
           kicked out                   No

Dec. 14    Hole in 6" pinch valve on
           first stage recycle line     No

Dec. 15    Leak on second stage dis-
           charge header                No
Dec. 15    Lost flow in "B" MgO pump     No

Dec. 16    Lost flow in "B" MgO pump     No
Dec. 16    Centrifuge hopper clogged     No
                                                                  Divert centrifuge; clean out

                                                                  Divert centrifuge; wash hopper
                                                         32 hrs.   Replace line
                                                         28 hrs.   Replace line
                                                                  Reset
                                                                  Repaired Dec. 16
                                                                  Switch to "A" pump; clean out "B" pump

                                                                  Backflush pump
                                                                  Divert centrifuge; wash hopper

-------
 I
•n
M
o
 I
                       Type of              Shut-down  Duration
        Date         Malfunction            Required   of Outage

       Dec.  17     Hole in  first  stage of
                  scrubber vessel               No
       Dec.  17     pH meter clogged with
                  crystals                     No
       Dec.  17     Leak in  second stage dis-
                  charge header                 No

       Dec.  18     Dryer conveyor tripped        No
       Dec.  18     Another  leak in second
                  stage discharge header        No
       Dec.  18     Dryer clogged                 No
Dec. 19    Failure of second  stage
           discharge header pipe         Yes      2% hrs.
Dec. 19    "C" MgO pump clogged           No
Dec. 19    Dryer conveyor tipped         No
Dec. 19    Leak in first stage scrubber
           vessel                        No

Dec. 20    Leak in first stage reducer    No
Dec. 20    Front rappers on dryer not
           hitting                       No

Dec. 20    Leak in line to upper pond     No

Dec. 21    Leaks on two of the first
           stage nozzle lines            No
Dec. 21    Leak in 8" pinch valve liner           1 hr.
           on first stage recycle line    Yes      10 man.

Dec. 22    Leak in first stage recycle
           line to plumb bob              No
                                                                  Remedial Action  Taken


                                                          Hole patched

                                                          Flush out

                                                          Repaired Dec. 19

                                                          Divert centrifuge; reset switch

                                                          Repaired Dec. 9
                                                          Cut back load and allow  dryer  to  clear
                                                          itself
Weld leak
Unclogged Dec. 30
Reset switch

Repaired Jan. 13

Temporary patch applied; welded on Dec. 21
Band couldn't be tightened; centrifuge
diverted until dryer cleared; repaired
on Jan. 11
Replaced with hose
                                                                 Leaks plugged
                                                                 Scrubber shut down on Dec. 22 to repair
                                                                 leak
                                                                 Welded, during Dec. 23 outage

-------
 Date

Dec. 23
     Type of
   Malfunction
Shut-down
Required
l.Leak in 8" pinch valve
  on first stage recycle
  line                        Yes
2.Leak in second stage dis-
  charge line
Dec. 26    pH meter not working          No

Dec. 28    Centrifuge hopper clogged.     No
Dec. 28    Leak in elbow of "A" first
           stage pump                    No
Dec. 28    Leak at pH meter electrode    No

Dec. 29    Bucket elevator tripped       No
Dec. 29    Leak in elbow of "A" first
           stage pump                    Yes
Dec. 29    Leak in elbow of "A" first
           stage pump                    Yes
Jan. H-     3" drain at bottom of scrubber
           plugged                       No
Jan. 4     Leak in second stage drain
           connection                    Yes

Jan. 8     Leak in elbow of "B" dis-
           charge pump                   Yes

Jan.10     Leaks in second stage lines   Yes

Jan. 11    MgO belt slipping             No
Jan. 11    MgO steam sparger clogged     No
Jan. 11    Leak in centrifuge cover      No
Duration
of Outage

 3 days
 12 hrs.
 40 min.
                                      15 min.

                                      4 days
                                      22 3/4
                                       hrs.
                                      3 days
                                      9 hrs.
                                      2 hrs.

                                      28 hrs.
Remedial Action Taken
                                                           1.  Replaced  with spool  piece
                                                           2.  Leak welded
                     Remove restriction from line

                     Divert centrifuge; wash hopper

                     Leak plugged
                     Leak plugged

                     Dug out boot; reset elevator

                     Leak plugged
                     Leak required only 15 minutes to repair,
                     but fan would not start.  It was de-
                     cided to leave the scrubber off so
                     other repairs could be made.
                     Unplug during shutdown

                     Leak repaired


                     Leak repaired

                     Inspect, repair and replace lines

                     Belt tightened
                     Cleaned

-------
CO
I
                Type of              Shut-down
 Date         Malfunction            Required

Jan. 12    "A" MgO pump failure          No

Jan. 13    SOp analyzer outlet probe
           clogged                       No

Jan. 13    MgO weigh feeder incorrect    No
Jan. 13    Another leak in centrifuge
           cover                         No

Jan. 14    Centrifuge hopper clogged     No

Jan. 1U-    First stage level controller
           frozen                        No

Jan. 14-    "A" thickener underflow pump
           and. rotometer frozen          No
Jan. 14    Run out of MgO                Yes
        Jan.  18    MgS03 conveyor at top of
                  silo kicked out               Yes*
        Jan. 19    Leak in liner of first
                  stage bleed valve             No
        Jan. 19    Oil leaking from mother
                  liquor agitator gear box      No
        Jan. 19    First stage overflow          Yes
        Jan.  23     First stage bleed lines
                   semi restricted               No
        Jan.  23     MgO weigh feeder belt
                   slipping                      No
                                                        Duration
                                                        of Outage
                                                        3 days
                                                        20% hrs.
                                                 4 days
                                                 45 min.
        Remedial Action Taken

Switch to "B" pump
                                                                  Stainless steel bands and tubing need
                                                                  to be replaced
                                                                  Recalibrate
                                                                  Divert centrifuge; wash hopper; use
                                                                  vibrators constantly

                                                                  Manual control used until controls
                                                                  unfrozen
                                                                                                            i
                                                                  Pump was cleared; rotometer to be replaced;
*Unable to inspect or fix due to icy
conditions on platforms.  Conveyor
freed when conditions permitted.

Removed metal pieces from valve; no
replacement liner available.

Refilled with oil
Remove restriction from first stage
bleed line

Both thickeners put in operation to get
more flow to the dilution tank
Cut back fan amps so MgO could catch
up

-------
 Date

Jan. 24

Jan. 24

Jan. 24
Jan. 24
Jan. 24


Jan. 25



Jan. 27

Jan. 27
Aug. 11

Aug. 11

Aug. 15
Aug. 24
Aug. 24
Aug. 24
                Type of              Shut-down
              Malfunction            Required

           Leak in first stage
           tangential spray header       No
           Leak in first stage
           torus spray                   No
           Centrifuge hopper clogged     No
           Bucket elevator  tripped       No
           Leak in 10"  header at  top
           of scrubber                   No

           Leak in 10"  header at  top
           of scrubber                   Yes*
           Inlet damper for Mode  II
           would not open                 No
           Restriction in  first stage
           pump "A"                      No*
First stage bleed valve liner
failure                       No
Cracked steam control valve   No
                                     Duration
                                     of Outage
Dryer Clogging
Dryer Clogging
Bucket elevator tripped
Excessive centrifuge
vibration
Aug. 26   . Wet centrifuge cake
Yes


No
No

Yes

Yes*
                                      38%
                                      hrs.
                                                 7  days
                                                 10%  hrs.
                          Remedial  Action Taken
                  Patched during boiler outage

                  Patched during boiler outage
                  Divert centrifuge;  wash hopper
                  V-Belts on  top of elevator replaced

                  Patch leak

                  *Shut down  to  patch leak and  to  save
                  wear on the system  as visitors are ex-
                  pected on Jan.  27
                                               Damper opened with aid of a crow-bar.
                                               *Shut down shortly after.  Restriction
                                               was a broken off  tangential nozzle.
                                               Scrubber to be kept off until after
                                               a  scheduled boiler outage.
Replaced Aug. 12
Replaced with spool piece on Aug. 14

Clean dryer manually
                                                          Remove build up manually
                                                          Reset elevator
                                                 37%  hrs.  Repairs made to centrifuge

                                                          *First stage only; weir height on
                                                          centrifuge lowered

-------
 Date

Aug. 27



Sept. 19

Oct. 20
     Type of
   Maitunerion

Leak in first stage
recycle lines
Gear box failure in
"A" thickener
Pins sheared in centrifuge
Shut-down  Duration
Required.   of
    Yes



    No

    Yes
days   Replace lines
                                       4% hrs.
                                                 Final
       "B" thickener only used

        None

-------
       LIST OF




SCRUBBER MAINTENANCE
          -F15-

-------
Oct., 9    1.  "A" underflow booster pump installed

Oct. 11   1.  Inboard bucket elevator bearing to be greased
              once per day.
          2.  Outboard bucket elevator bearings to  be greased
              once per week.
          3.  Silo vibrator motors to be greased once every
              three months.
          4.  All unused pumps and the centrifuge (when not
              in use) shall be bumped at least once per day.

Oct. 15   1.  Silo vibrator motor replaced.

Oct. 18
  to
Oct. 21   1.  Inspect MgO slurry flow meter.

Oct. 22   1.  Boulders of MgO broken up in silo.

Oct. 25   1.  Electricians adjust vibrator times; install
              toggle switches for manual operation.

Oct. 27   1.  A detailed inspection/lubrication program was
              initiated by Chemico personnel  to be  performed
              during the 4-12 shift.  The program consisted
              of inspecting/lubricating the following:

          Thickener Area -

          1.  Transfer pump bearing pedestals
          2.  Underflow pump bearing cases.
          3.  Underflow booster bearing cases.
          4.  Dilution tank gear reducer-agitator.
          5.  Dilution tank agitator bearings.
          6.  Thickener rake drive gears.
          7.  Thickener rake lift gears.
          8.  Dry er

              A.  Lubricate tires
              B.  Lubricate trunions
              C.  Lubricate thrust bearings
              D.  Oil drive gear case
                              -F16-

-------
          Scrubber Area -

          1.  ID fan motor oil levels
          2.  ID fan fluid drive oil levels
          3.  ID fan bearings oil
          4.  ID fan boiley controllers
          5.  First stage pumps-motors oil level
          6.  First stage pumps-bearings oil level
          7.  Second stage pumps-bearings oil level
          8.  Dryer ID fan-bearings lubricate
          9.  Dryer ID fan-bailey controller lubricate
         10e  #4 conveyor (top silo) bearings and reducer
         11.  Bucket elevator bearings and reducer
         12.  Plumb bob limitorque gear reducer

          Dryer Area -

          1.  #1 conveyor bearings and gear reducer
          2.  #2 conveyor bearings and gear reducer
          3.  Dryer conveyor bearings and gear reducer
          4.  Centrifuge reservoir and bearings
          5.  Stack damper (dryer) lubricate
          6.  Premix tank agitator bearing lubricate
          7.  MgO mix tank agitator gear reducer
          8.  Mother Liquor tank agitator gear reducer
          9.  MgO pumps bearing oil
         10.  Mother Liquor pumps bearing oil
         11.  Bottom bucket elevator four bearings (weekly)

Oct. 27
  to
Nov. 11   1.  Clean out valves on "A" MgO pump dicharge line
              installed.
          2.  The level in the MgO silo was measured.
          3.  The ID fan was inspected.
          4-.  Dryer rappers were adjusted.
          5.  Rappers on the centrifuge hopper were
              relocated.
          6.  A new motor was installed on the dryer
              conveyor.
          7.  Vibrator installed on the MgSOg silo so
              sticking would not occur.
          8.  First stage cone was opened and inspected.
          9.  Bucket elevator bearings were inspected  and
              lubricated; one was replaced.
         10.  Weigh belts were zeroed and calibrated.
         11.  Electricians installed a larger heater in
              the "B" MgO pump switch.
                               -F17-

-------
Nov. 11   1.  Temperature monitors on fire box and steam
  to          control valves were serviced.
Nov. 13   2.  The thermocouple on the circulation line was
              repositioned for more effective control.
          3.  Flow rate checks on the MgO slurry lines.

Nov. 18   1.  Hub on the dryer screw conveyor was inspected
  to          and replaced.
Nov. 19   2.  The liner on the centrifuge divert valve was
              inspected and replaced.

Nov. 22   1.  Electrician removed the inspection plate from
              the dryer. ID fan wouldn't start and discovered
              the housing one-half filled with water.  After
              draining the housing, the pulley hub was in-
              spected and found to be worn.
          2.  Inspected bearings on dryer screw conveyor.

Nov. 25   1.  pH controller serviced.

Dec. 3    1.  Removed one stellited restricting orifice plate
  to          from the first stage bleed line to the thickener.
Dec. 5

Dec. 6    1.  Removed the three remaining stellited restrict-
              ing orifice plates from the first stage bleed
              line.
          2.  DuPont SOj analyzer serviced.

Dec. 9    1.  Oilers on vibrators serviced.

Dec. 10   1.  Overload heaters installed in "B" MgO pump.

Dec. 12   1.  "A" thickener rakes were inspected.

Dec. 13   1.  Inspected first stage bleed line for restrictions.

Dec. 11   1.  Removed and inspected motor on Mother Liquor
              agitator; gears need replacement.

Dec. 16   1.  Larger overload heaters installed, in "B"
              second stage pump.

Dec. 17   1.  Blanks were installed in the tangential nozzle
              lines to prevent leaks.

Dec, 23   1.  Inspected screens in the MgO tank.
  to      2.  Pre-mix tank cleaned.
Dec. 26
                             -F18--

-------
Dec. 27   1.  Pipe thickness measurements made.
          2.  Adjusted packing on first stage and
              transfer pumps.

Dec. 29   1.  inside of the second stage vessel  inspected.
  to      2.  Drain valves installed on the casings of
Jan. 3        "B" and "C" MgO pumps.
          3.  Top mist eliminator washed.

Jan. 6    1.  Second stage vessel checked for leaks.
  to
Jan. 7

Jan. 10   1.  During the past week, all equipment requiring
              lubrication was serviced.

Jan. 15   1.  Repacked both first stage recycle pumps.
  to      2.  Calibrate level controllers.
Jan. 18   3.  New buckets installed on MgSC>3 elevator.
          4.  Rotometers thawed and insulated as needed.
          5.  Clean out MgO pre-mix tank.
          6.  Inspect, clean and grease steam sparger valve.
          7.  Cleaned guages on MgO pumps.
          8.  pH meter pot serviced.
          9.  "B" first stage pump taken apart to remove
              an 18" section of tangential nozzle.
         10.  Inspected tangential nozzles; 6 of 10 missing.

Jan. 19   1.  Removed two of the remaining four  tangential
  to          spray nozzles from the first stage.
Jan. 23   2.  All pumps fully opened to prevent  freezing.
          3.  First stage discharge header drained to
              prevent freezing.

Jan. 25   1.  First stage recycle pumps jumpered so they
              could be stopped without tripping the ID fan.

Jan. 26   1.  New V-belts installed at the top of the MgS03
              bucket elevator.

Aug. 24   1.  Inspection of inside of first stage vessel.

Sept. 19  1.  Inspect bucket elevator and tighten buckets if
              needed.
                             -FID--

-------
                                TECHNICAL REPORT DATA
                         /Please read Instructions on the reverse before completing)
1. HEPOHTNO.
  EPA-600/2-7'f-165
                           2.
                                                      3. RECIPIENT'S ACCESSION-NO.
4, "ITLE AND SUBTITLE
Magnesia FGD Process Testing on a Coal-Fired
   Power Plant
                              8. REPORT DATE
                               August 1977
                              6. PERFORMING ORGANIZATION CODE
7. AUTHOR(S)

Diane K. Sommerer
                                                      8. PERFORMING ORGANIZATION REPORT NO.
                               Y-8479
9. PERFORMING OROAMZATION NAME AND ADDRESS
York Research Corporation
One Research Drive
Si:amford, Connecticut  06906
                              10. PROGRAM ELEMENT NO.

                               1AB013; ROAP 21BAV
                              11. CONTRACT/GRANT NO.
                               68-02-1401, Tasks 1,10,24,
                                and 25
12 SPONSORING AGENCY NAME AND ADDRESS
                                                                      D PERIOD COVERED
 EPA, Office oi Research and Development
 Industrial Environmental Research Laboratory
 Research Triangle Park, NC 27711
                              13. TYPE OF REPORT AND PERIOD
                              Task Final; 10/74-8/75
                              14. SPONSORING AGENCY CODE
                                EPA/600/13
is SUPPLEMENTARY NOTES IERL_RTP pr0ject officer for this report is C. J.Chatlynne, Mail
Erop 61, 919/541-2915.
16. ABSTRACT
               repOrt gives results of a field measurement program to determine the
operability and reliability of the Chemico magnesium oxide ventuo scrubber operating
at Potomac Electric Power Company's Dickerson Generating Station, Frederick , MD.
A continuous source-monitoring station was installed at the scrubber, complemented
by a field analytical laboratory intended for the measurement and analysis of various
process streams. These facilities continuously monitored process and emission
variables between October 1974 and January 1975, and during August 1975.  Scrubber
operation .was evaluated during steady-state and transient operation, the latter inclu-
ding startups,  shutdowns, and malfunctions. During the tests, the scrubber was avail1-
able about 48% of the time, including all levels of operation. Approximately 80% of
system availability- was  steady-state, with the system operating normally. The  tests
showed that, although scrubber availability was not ideal (due to logistics problems
m supplying raw materials (MgO) , and to mechanical problems mainly attributable
to under-design in such  areas  as piping, slurry pumps, and other auxiliary equip-
ment),  the basic scrubber concent and design should meet critical criteria once these
problems are remedied.
17.
                             KEY WORDS AND DOCUMENT ANALYSIS
                DESCRIPTORS
                                          b.IDENTIFIERS/OPEN ENDED TERMS
                                           c.  COSATI Field/Group
Air Pollution
Flue Gases
Desulfurizatiori
Magnesium Gxudes
Scrubbers
Venturi Tubes
Coal
Combustion
Electric Power
  Plants
Air Pollution Control
Stationary Sources
13B
21B
07A,07D
07B

14B
21D
18. DISTRIBUTION STATEMENT

 Unlimited
                  19. SECURITY CLASS (This Report)
                  Unclassified
                        21. NO. OF PAGES
                             264
                  20. SECURITY CLASS (This page)
                  Unclassified
                        22. PRICE
EFA Form 2220-1 (9-73)
                                      -F20-

-------