Environmental Protection Technology Series
INVESTIGATION  OF REUSE POTENTIAL
  OF ASH FROM PAPERMILL  SLUDGES
                  Industrial Environmentai Research Laboratory
                       Office of Research and Development
                      U.S. Environmental Protection Agency
                               Cincinnati, Ohio 45268

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                 RESEARCH REPORTING SERIES

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 Protection Agency, have been grouped into nine series. These nine broad cate-
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 This report has  been assigned  to the ENVIRONMENTAL PROTECTION TECH-
 NOLOGY series. This series describes research performed to develop and dem-
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This document is available to the public through the National Technical Informa-
tion Service, Springfield, Virginia  22161.

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                                           EPA-600/2-77-123
                                           July 1977
            INVESTIGATION OF REUSE  POTENTIAL

             OF ASH FROM PAPERMILL  SLUDGES


                           by
                   Allan M.  Springer
                   Duane W.  Marshall
         National Council of the Paper Industry
          for Air and Stream Improvement, Inc.
           Central-Lake States Regional Center
             Kalamazoo, Michigan   49008
                    Isaiah Gellman
         National Council of the Paper Industry
          for Air and Stream Improvement, Inc.
              New York, New York   10016
               Grant No. EPA-R-803348-01
                    Project Officer

                   Victor J. Dallons
         Industrial Pollution Control Division
Industrial Environmental Research Laboratory-Cincinnati
               Corvallis, Oregon   97330
     INDUSTRIAL ENVIRONMENTAL RESEARCH LABORATORY
           OFFICE OF RESEARCH AND DEVELOPMENT
         U.S. ENVIRONMENTAL PROTECTION AGENCY
                CINCINNATI, OHIO  45268

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                           DISCLAIMER
     This report has been reviewed by the Industrial Environ-
mental Research Laboratory, U.S. Environmental Protection Agency,
and approved for publication.  Approval does not signify that the
contents necessarily reflect the views and policies of the U.S.
Environmental Protection Agency, nor does mention of trade names
or commercial products constitute endorsement or recommendation
for use.

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                            FOREWORD
 When energy and material  resources  are  extracted,  processed,
 converted,  and used,  the  related pollutional  impacts  on  our
 environment and even  on our health  often  require that new
 and increasingly more efficient pollution control  methods be
.used.   The  Industrial Environmental Research  Laboratory  -
 Cincinnati  (lERL-Ci)  assists in developing and demonstrating
 new and improved methodologies  that will  meet these needs
 both efficiently and  economically.

 "Investigation of Reuse Potential of Ash  From Papermill  Sludges"
 is  a product of the above efforts.   Two techniques for
 recovery of filler from fine papermill  high ash sludges,
 screening and wet oxidation, were evaluated for their technical
 feasibility.   The alternative of screening the sludge and using
 the material passing  through the screen as recovered  filler
 was investigated in cooperation with two  mills.  The  wet
 oxidation scheme appears  technically feasible. The screening
 alternative would probably have to  incorporate a bleaching
 step before it would  be deemed  acceptable. The technical
 feasibility of oxidative  bleaching  was  demonstrated.

 For further information regarding this  report contact the
 Food and Wood Products Branch,  Industrial Pollution Control
 Division, Industrial  Environmental  Research Laboratory—Ci,
 Cincinnati, Ohio  45268.
                        David G.  Stephan
                            Director
        Industrial Environmental  Research Laboratory—Ci
                        Cincinnati,  Ohio
                               111

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                            ABSTRACT


     Two techniques for recovery of filler from fine papermill
high ash sludges, screening and wet oxidation, were evaluated for
their technical feasibility.  The alternative of screening the
sludge and using the material passing through the screen as
recovered filler was investigated in cooperation with two mills.
The screening for recovery of filler was conducted at the mill
site.  Then the material was shipped to Western Michigan Univer-
sity where selected grades incorporating the recovered filler
were manufactured.  The paper manufactured was shipped to Roches-
ter Institute of Technology where it was printed on their web
offset press.  The grades simulated were found lacking only in
that the brightness of the paper was from four to seven points
lower than grades made with virgin filler.  The wet oxidation
alternative was evaluated in a similar manner with a cooperating
mill.  The wet oxidized, recovered fillers only slightly lowered
the brightness of the sheet simulated and gave an increase in
opacity in exchange.  The wet oxidation scheme appears techni-
cally feasible.  The screening alternative would probably have
to incorporate a bleaching step before it would be deemed accept-
able.  The technical feasibility of oxidative bleaching was
demonstrated.
                               IV

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                            CONTENTS
Foreword                                                     iii

Abstract                                                      iv

List of Figures                                               vi

List of Tables                                               vii

Acknowledgments                                               ix

I      Conclusions                                             1

II     Recommendations                                         3

III    Introduction                                            4

IV     Evaluation of Screening as a Recovery Alternative       8
       for a Mill Manufacturing Coated Fine Paper

V      Discussion of Results from Evaluation of               13
       Screening as an Alternative for Filler
       Recovery from High Ash Sludge for Reuse in
       Coated Fine Paper

VI     Evaluation of Screening as a Recovery Alternative      21
       for a Mill Manufacturing Uncoated Fine Paper

VII    Discussion of Results                                  26

VIII   Bleaching of Screened, Recovered Filler                36

IX     Plausible Screening System to Recover Filler           39

X      Evaluation of Filler Recovered by Wet Oxidation        47

XI     Discussion of Results for Use of Wet Oxidized          50
       Recovered Filler as a Filler Pigment

XII    Potential of Wet Oxidized, Recovered Filler as a       56
       Possible Coating Pigment

XIII   References                                             58

XIV    Appendices                                             59

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                        LIST OF FIGURES


Number                                                      Page

  1    Full Scale Pigment Recovery System                      6

  2    Diagram of Possible Scheme for Mill Installation       40

  3    Case I Primary Clarifier Sludge Utilization            44
       Bleaching System

  4    Acid Demand of Wet Oxidized Pigment                    51

  5    Particle Size Distribution of Wet Oxidized             57
       Recovered Filler

  1-A  Foam Flotation:  Time vs. % Filler Purity and          67
       Recovery

  2-A  Screening - The Effect of Screen Mesh and              69
       Consistency on Purity and Recovery
                               VI

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                         LIST OF TABLES


Number                                                      Page

  1    Screening Characteristics for Filler Recovery          14
       for Reuse in Coated Fine Paper

  2    Physical and Optical Properties of Coating             15
       Base Sheet

  3    Coated Offset Sheet Physical Properties                17

  4    Coated Offset Sheet Optical Properties                 18

  5    Coated Offset Sheet Laboratory Printing Tests          18

  6    Coated Offset Sheet Printing Results                   20

  7    Comparison of Laboratory Screening vs. Mill            27
       Site Screening of Conventional High Ash Sludge

  8    Uncoated Offset Model Machine Trial Retention          28
       Values

  9    Uncoated Offset Sheet Physical Properties              29

 10    Uncoated Offset Sheet Optical Properties               31

 11    Uncoated Offset Sheet Laboratory Printing              32
       Properties

 12    Evaluation of Web Offset Printed Samples               34

 13    Printing Sharpness of Sequential Samples               35

 14    Conditions for Bleaching                               37

 15    Bleaching Results                                      38

 16    Bleaching Conditions for Mill Reclaiming               46
       Clarifier Sludge by Processing Through Bleach
       Plant
                              Vll

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                         LIST OF TABLES
                          (continued)


N limber                                                      Page

 17    Characteristics of Filler Recovered by Wet             50
       Oxidation of Deinking Sludge

 18    Retention Characteristics of Wet Oxidized              52
       Recovered Filler

 19    Wet Oxidized, Recovered Filler Uncoated Offset         53
       Paper Physical Properties

 20    Wet Oxidized, Recovered Filler Uncoated Offset         54
       Paper Optical Properties

 21    Wet Oxidized, Recovered Filler Uncoated Offset         54
       Paper Printing Properties

 22    Uncoated Offset Sheet Printing Results                 55

 1-A   Recovered Filler Purities from Centrifugal             64
       Separation Deinking Sludge

 2-A   Recovered Filler Purities from Centrifugal             65
       Separation Conventional Sludge

 3-A   Summary of High Ash Sludge Laboratory Recovery         66
       Technique Data - Purity

 4-A   Summary of High Ash Sludge Laboratory Recovery         66
       Technique Data - Recovery

 5-A   Brightness Results                                     70

 6-A   Abrasion Results by Flat Disc Method                   70

 7-A   Hand Sheet Properties Modification (Conventional)       72

 8-A   Hand Sheet Properties Modification (Deinking)           73

 1-D   Printing Sample Evaluation by Use of 1-5 Grading       83
       System


                              viii

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                        ACKNOWLEDGMENTS
     The Project Engineer, Dr. A.M. Springer, wishes to acknow-
ledge the following organizations and their personnel, particu-
larly those cited, whose assistance and cooperation was indis-
pensable to the conduct of this study:
     Allied Paper Company
     Bergstrom Paper Company

     Consolidated Paper Company
     Fletcher Paper Company
Mr. F. Harrison
Mr. L. Stoeffler
Mr. M. Smith
Mr. J. Stiegemeyer

Mr. Ken Maves

Dr. I Sanborn
Mr. P- Cox
Mr. R. Lau
Mr. D. Rucks
Mr. J. Uttermark

Mr. Ed Grys
     Rochester Institute of Technology    Mr. R. McAllen
     Western Michigan University
     Zimpro Inc.
Mr. H. Warren
Mr. C. Schuster
Mr. K. Many on
Dr. W.E. Rayford

Mr. Bernard Flynn
Mr. Chuck Soukup
     The efforts of the NCASI technician staff, especially the
help of Mr. T. Arnson, Mrs. D. Trainer and Mr. J. Marks, and the
secretarial assistance of Mrs. E. Kavelman was most appreciated.

     The guidance provided by the NCASI technical staff, namely
Dr. I. Gellman, Mr. R. Blosser and Mr. D. Marshall, was also
appreciated.

     Finally, the support of this study by the Office of Re-
search and Development of the United States Environmental Pro-
tection Agency,  and the assistance provided by the Project Offi-
cer, Mr.  V. Dallons,  is gratefully acknowledged.
                               IX

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                           SECTION I

                          CONCLUSIONS


     Fractionation of the high ash sludge from the primary clari-
fier of a fine paper manufacturing operation by use of a vibra-
ting screen results in a reusable high filler content fraction,
which passes through the screen, and a high organic material
content fraction, which is retained on the screen.  The high or-
ganic content fraction becomes amenable to incineration, should
circumstances dictate.  Fifty to seventy-five percent of the
sludge may be reclaimed in the high ash fraction as possible
reusable material and would result in a parallel decrease in the
mass of sludge requiring disposal.

     In recovery of fillers in the paper manufacturing process,
selection of screen mesh and feed rate are specific to each mill
due to the varying nature of the sludges and the tolerance of
the mill's grade structure to contamination introduced with the
recovered materials.  In the course of this study, a mill manu-
facturing coating base stock opted for a 100-mesh screen whereas
the mill making uncoated fine paper opted for a 230-mesh screen.
Less organic contamination is associated with the use of a finer
screen mesh.  However,- a smaller amount of material is recovered.

     Based upon pilot work, the screened, recovered filler did
not affect the physical properties of the sheet made in this
study when used to partially replace virgin filler.  The highest
level of replacement observed was 83 percent of the filler clay,
constituting 68 percent of the total filler.  The screened,
recovered filler did not (a) affect the printing properties of
the sheet in the grades examined, (b) increase the dirt count of
the sheets or (c) adversely affect the filler retention charac-
teristics of the pilot paper machine.  Moreover, the recovered
materials have abrasive properties comparable to normal filler
grade clay utilized in the paper industry.

     Utilization of screened, recovered filler led to an increase
in opacity of the sheets.  The 50-lb (74 gm/m2) coated offset
grade gained 3.6 points in the base stock and 1.8 points in the
final coated product.  The 50-lb  (74 gm/m2) uncoated offset sheet
gained 1.2 points and the 30-Ib sheet  (44 gm/m2), 0.4 points.

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     Utilization of screened, recovered filler, however, did ad-
versely affect the brightness of the sheets.  For the 50-lb
(74 gm/m2) coated offset grade, this amounted to 7 points in the
coating base sheets; 4 points in the final coated sheet.  For the
uncoated offset sheet, it amounted to 4.6 points for the 50-lb
(74 gm/m2) sheet and 0.8 of a point for the 30-lb (44 gm/m2)
sheet.  All sheets reflected deteriorating brightness, with dif-
ferences in magnitude attributable to utilization of  (a) differ-
ent sludges, (b) differing media for screening, (c)  different
levels of addition of the recovered filler and  (d)  different
blends of filler materials.  Subsequent study indicates that oxi-
dative bleaching techniques have potential for brightening
screened, recovered filler.

     Wet oxidation produces a reusable filler material from high
ash sludges.  Fillers recovered by wet oxidation did not
(a) harm the physical properties of the sheet,  (b)  increase the
dirt count of the sheet, or  (c) adversely affect the printing
properties of the sheet at addition levels employed in this
study.  Futhermore, tests of the wet oxidized, recovered filler
indicated it to be no more abrasive than normal filler clay.

     The wet oxidized, recovered filler from the sludge evalu-
ated imparted 2.6 points lower brightness to the sheet but gave
an increased 4.9 points of opacity.  From the standpoint of
product brightness, wet oxidation would have to be considered
superior to separation by screening.  However,- the wet oxidized,
recovered filler from the sludge evaluated has a buffer effect
and consumed several times as much acid in controlling the pH
to 4.5 during the machine trial as did No. 2 coating clay when it
was used as filler.  In comparison with No. 2 coating clay,
titration of the wet oxidized filler from pH 7 to pH 4.5 required
48 times the quantity of sulfuric acid.

     The screening alternative looked more promising than wet
oxidation for the conventional mill  (nondeinking)  but would not
be feasible for the deinking mill due to the low brightness of
the recovered product.  The wet oxidation alternative would
appear workable on either type of sludge but involves a good deal
higher capital investment cost than the screening.

     The wet oxidized, recovered filler was preliminarily evalu-
ated as a coating pigment.  The evaluation showed that this
material would be unsuitable as a coating pigment due to its
heterogeneous nature, lower brightness, particle size distribu-
tion, and dispersion difficulties.

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                           SECTION II

                        RECOMMENDATIONS


     This study has addressed the technical feasibility for
recovery of filler materials from high ash sludges and subse-
quent reuse in the paper manufacturing process.   Though separa-
tion techniques employed herein involved screening and wet oxida-
tion, efforts were not made to optimize either.   As a consequence
alternative screening devices besides the Sweco  vibrating screen,
as well as alternative wet oxidation processes,  should be evalu-
ated for their relative merits as a means for filler recovery
from clarifier underflow.

     Remaining to be quantified are the operational and economic
implications of filler recovery on a larger scale continuous
basis.  Alternative means for filler recovery warrant further
evaluation on a continuously operating pilot plant scale at an
actual mill site.  Elements of such further study would appro-
priately include such issues as how the variable nature of the
clarifier underflow would affect properties of the recovered
filler and how much equilization capacity would be required to
dampen variation of those properties.  It could also address the
issue of system dependability and the effect of recovered filler
addition to a full scale paper machine system.  Cost analysis
would appropriately follow to determine the economic feasibility
of filler recovery by screening or wet oxidation in an overall
residuals management program.

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                          SECTION III

                          INTRODUCTION


     Among the solids which are accumulated in the treatment of
wastewaters of pulp and paper origin are those lost from the
papermaking process and subsequently separated during primary
clarification.  Land disposal is the largest single method prac-
ticed in the pulp and paper industry for disposal of these
sludges.  Sludges with ash contents exceeding 50 percent are
commonly associated with the manufacture of (a) deinked pulp and
paper and (b) integrated and nonintegrated fine papers.  In the
absence of by-product recovery opportunities, land disposal
remains the only feasible method of disposing of these sludges.
Of the mills which must deal with the disposal of high ash
sludges, more than 100 are located in or adjacent to metropolitan
areas where land available for solid waste disposal is limited.
Combined with declining land availability in restricting the
practice of land disposal are declining public acceptance and
increasingly stringent regulation.  Thus, an impetus for develop-
ment of by-product approaches is clearly suggested.

     This problem was identified as early as 1951 when the Kala-
mazoo River Improvement Company (a group of six paper companies
in southwestern Michigan practicing deinking)  initiated work
under the direction of Dr. A. H. Nadelman to develop alternative
solutions to the problem (1).  Two approaches were pursued: the
first to convert sludge into a product which could be reused on
site in the papermaking operation, and the second to study the
possibility of other industrial uses of the sludge.  Two pro-
cesses for sludge modification were investigated and included:
(a) drying and powdering and (b) calcining and ball milling the
sludge.

     The calcined product was of adequate brightness for reuse in
the papermaking process, though agglomerated.  As a consequence,
it was necessary to pulverize the reclaimed material with a ball
mill.  Though promising from the standpoint of appearance, the
final product, when evaluated for abrasiveness with the Valley
abrasion tester (2), was found to be more than 10 times as
abrasive as commercial clay, thus down-grading its desirability
as a paper filler material.  The material was also evaluated for
use as a filler pigment in rubber products and asphalt tile and
found to function satisfactorily.  However, for those

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applications the cost of calcining and ball milling made the
recovered fillers more expensive than virgin filler.

     Attention was, therefore, given to other techniques for
recovering the filler, including electrophoretic separation and
flotation.  Electrophoresis seemed an unlikely alternative since
the cost of electrical power needed to do the separation was
more than the value of the product produced.  Flotation, however,
was shown to have some potential for making a partial separation,
but experiments were not carried far enough to reach a definite
conclusion.

     In early 1962, S. D. Warren Company began development work
in the field of sludge incineration and arrived at a viable sys-
tem for their fine paper mills which they felt would economically
dispose of their primary high ash sludge while generating from
it a usable paper filler material.  A full scale system, which
was constructed and operated under an EPA demonstration grant,
is shown in Figure 1.  It consisted of (a) a centricleaner system
to remove grit, (b) vacuum filters to dewater the sludge, (c)  a
shredder to break up the cake, (d) a rotary kiln to incinerate
the sludge and (e) a pulverizer classifier to break up the incin-
erated product (3).  It was observed that if the kiln temperature
was below 1500°F  (816°C), the product did not achieve the desired
brightness.  However, if the kiln temperature exceeded 1600°F
(871°C), the product was exceedingly abrasive, even after pulver-
ization.  By maintaining kiln temperatures between 1500 to 1550°F
(816 to 843°C) with a 90-minute detention time, a product could
be obtained which had a G.E. brightness of 84 to 85 percent.
Moreover, it was only two to five times as abrasive as normal
filler clay.  Full scale paper machine trials employing the
recovered filler were subsequently conducted, and the paper was
commercially printed with no difficulties encountered.  Based
on 1971 prices, the recovered filler was estimated to cost
$50/ton to produce.  In comparison, virgin filler cost only $38/
ton and was not plagued with the abrasive properties.  However,
the costs associated with solid waste disposal at specific mill
sites would warrant inclusion in the economic balance.  Because
of the abrasive properties of fillers recovered by incineration,
alternative techniques for recovery of filler material from
high ash sludge continued to warrant investigation, again with
the aim of providing a product which could be reused at the mill
as a paper filler material.  As a result, in 1973 the National
Council of the Paper Industry for Air and Stream Improvement
(NCASI) studied four separation techniques under laboratory con-
ditions to attempt recovery of filler from high ash sludge.
These included (a) foam  flotation, (b) centrifugal separation
(centricleaning),  (c) screening and  (d) wet oxidation.  The
capability of each was judged on the basis of  (a) the degree of
separation  (proportion of the recovered product which is filler),
(b) recovery  (the proportion of the original filler in the sludge
which is recovered) and  (c) brightness of the final product in

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SLUDGE
  2.5% SOLIDS
         CENTRI CLEANERS
CONSISTENCY   &
REGULATOR
     DILUTION
       TANK
      PULVERIZER
       CLASSIFIER
                         POLYMER INJECTION
                              V
                           REJECTS TO
                      SECONDARY TREATMENT
                                                               2.2 MGD
                                                               FILTRATE TO
                                                               SECONDARY
                                                               TREATMENT
                                                       SLUDGE CONVEYOR
                                          SHREDDER










11
\u-— -



__ — - —


BULK
STORAGE
— • — -




mi
L
WAT

i
V
                                                    SLURRY
                                                     TANK
           Figure  1.  Full scale pigment recovery system.

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comparison to the original sludge.  Appendix A contains the re-
sults of these tests as well as details of the experiments.  Two
high ash sludge samples were studied:  one from a fine paper mill
practicing deinking and one from a mill not deinking, which will
be termed a conventional mill.  The recovered fillers were eval-
uated for abrasiveness by a modification of the flat disc method
(4,5) and found to be nonabrasive.  Based upon this evaluation,
the screening and wet oxidation techniques showed most promise.
Further demonstration of the acceptability of filler materials
recovered by these techniques for reuse in the paper manufactur-
ing process required pilot plant scale trials.  To that end, it
was proposed to evaluate on pilot scale paper manufacturing
equipment the technical feasibility of reusing filler materials
recovered by the screening of sludges from two fine paper mills
and the wet oxidation of a third sludge generated at a fine
paper mill employing deinking.  In the course of doing so, the
screening alternative was evaluated for both coated and uncoated
grades of web offset printing paper, whereas the wet oxidation
alternative was evaluated only for uncoated web offset printing
paper.

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                           SECTION IV

             EVALUATION OF SCREENING AS A RECOVERY

     ALTERNATIVE FOR A MILL MANUFACTURING COATED FINE PAPER


EXPERIMENTAL DESIGN

     The overall experimental design involves simulating on a
model paper machine production of grades of pape^ similar to
those produced at cooperative mills, using both virgin and
reclaimed fillers, and testing the papers to distinguish property
changes due to reclaimed filler content.  In evaluating the po-
tential use of recovered fillers in the manufacture of coated
fine paper, a cooperative mill chose from its grade structure a
high volume grade felt to be capable of accepting recovered fil-
ler as part of its furnish.  In the normal production of this
particular grade, all of the filler normally employed in the
sheet enters in the coated broke.  Thus, recovered filler addi-
tion would increase the ash content of the grade.

     Utilizing virgin material provided by the mill, manufacture
of coated fine paper was simulated on a 24-in. (0.6 m) pilot
fourdrinier paper machine at Western Michigan University (WMU)
at the normal ash level of 5 percent, as well as a higher 8 per-
cent level representative of the ash content associated with
projected use of recovered fillers.  These sheets were compared
with a similarly manufactured sheet containing a combination of
virgin filler at the 5 percent level and sufficient recovered
filler to increase the ash content to 8 percent, thereby simu-
lating the way in which the mill would utilize the recovered
filler.

     The rolls of paper manufactured were shipped to the cooper-
ating mill to be coated and supercalendered.  The coated paper
was subsequently evaluated for its physical and optical proper-
ties and shipped to Rochester Institute of Technology for print-
ing on a commercial four-color web offset press.


SCREENING PROCEDURE

     The screening was accomplished at the research and develop-
ment center of the cooperating mill using a 30 in. (0.76 m)
diameter Sweco vibrating screen.  The primary clarifier sludge

                                8

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was trucked from the mill in drums, diluted to 2 percent, and
screened using a 100-mesh sieve.

     Mill personnel had previously conducted studies varying the
mesh size from 325 mesh to 100 mesh.  Initial examination of the
recovered fillers for brightness and dirt speck content suggested
that the separation effected by the 100-mesh screen would result
in an acceptable quality material for the intended end use.
Apparently a significant proportion of the dirt and grit were
preferentially retained on the screen with the more highly fi-
brous organic fraction, allowing a more selective passage of
filler components through the sieve.

     Furthermore, the 100-mesh screen had the added advantages
of (a)  allowing a higher throughput rate, 2 to 3 gpm (7.6 to
11.4 &/m) and (b) recovering a larger fraction of the clarifier
underflow as reusable material.  The recovered fraction, which
passed through the screen, amounted to 50 to 75 percent of the
total sludge.  Seventy to eighty-five percent of the possible
filler was recovered.  The recovered filler was thickened by
settling and decanted to approximately 5 to 8 percent solids.
In addition, it was treated with a biocide, 125 mg/S, Dowicide G,
to prevent bacterial degradation during subsequent shipment to
Western Michigan University-  There it was refrigerated upon
arrival.
PILOT PAPER MACHINE TRIAL

     The major raw materials for the pilot machine trial were
provided by the cooperating mill.  The groundwood pulp was
dewatered on a large vacuum screen to approximately 18 percent
solids and packed in polyethylene lined 55-gallon (210 I) drums
for shipment.  Pulp degradation was prevented by addition of
Rx-28.  The softwood kraft pulp was shipped in dry lap form to
Western Michigan University.  The starch (Cato 16)  and No. 2
coating clay were shipped in dry form in 100-lb  (45.4 Kg) bags.
Coating clay was utilized because in the mill the ash content in
the grade comes from addition of coated broke.

     A run with a 1-day machine trial was devoted to each of
three conditions designed to simulate  (a) the usual manner in
which the selected grade was produced in the mill, (b) the way
the grade would be manufactured if recovered fillers were to be
incorporated and (c) a control where the recovered filler was
replaced by virgin filler.

     In each case, the furnish was held constant throughout the
run at 45 percent groundwood and 55 percent softwood kraft.  The
softwood kraft was refined from 660 Canadian Standard Freeness
to 600 Canadian Standard Freeness  (CSF) in a beater.  The pres-
sure was then taken off the bed, and the groundwood was  added

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and  reslushed.   The  starch was  cooked  at  200°F  (93°C) for 30
minutes  at  6  percent solids  and diluted to  3 percent solids for
metering to the  machine.  The clay,  recovered filler, and starch
were metered  in  continuously to a  mix  tank  just before the head-
box.

     Distinctions  between the various  trials merit mention.  Dur-
ing  the  first trial, the starch was  metered in to give 1.75 per-
cent starch.  The  No.  2 coating clay was  slurried at 70 percent
solids,  diluted  to 15  percent solids,  and metered in at a rate
to give  5 percent  ash  in the sheet.  In the second trial, the
starch feed rate was increased  to  give 2.25 percent starch, but
the  virgin  clay  feed rate remained at  the previous day's level.
The  recovered filler,  at 3 percent consistency, was metered in
at a sufficient  rate to result  in  a  final ash level in the sheet
of 8 percent.  In  the  final  trial  on the  third day, the starch
level was left fixed at the  previous day's  level.  However,
recovered filler was not used and  the  feed  rate of virgin filler
was  increased to yield an ash content  of  8  percent.  The recov-
ered filler was  replaced exactly with  virgin filler.

     Throughout  the  trials the  basis weight was held constant at
45 lb/3300  ft2 (66.6 gm/m2) .  The  alum level was maintained at
30 Ib/ton (15 Kg/metric ton) .   All water  used in the trial was
deionized.  Hardness was added  back  to' give 200 grains (3420 mg/
£) .  The headbox temperature was maintained at 95QF (35°C) , and
headbox  pH  was adjusted continuously with sulfuric acid to give
a pH of  4.5 to 4.7.  The sheet  was not internally sized nor was
a size press  used.   Three nips  were  used  in the calender stack.
The  dandy roll was not used.  The  final sheet moisture was con-
trolled  to  3  percent ± 0.5 percent.

     During the  run, the basis  weight  and moisture were con-
trolled  by  the machine's Accu-ray  system.   Four times during each
day's run 30-ft  (9.1 m) paper samples  were  collected and stored
in a constant temperature and humidity control testing laboratory
for  later evaluation.  Concurrently  control tests for basis
weight,  caliper, ash,  and Scott Bond were conducted.  The col-
lected paper  samples were subsequently cut  every 2 feet (0.6 m)
for  a length  of  20 feet (6.1 m)  to provide  10 segments for test-
ing  each of the  physical, optical  and  printing properties of
interest.   For each  test, a  strip  from each of the 10 samples
was  evaluated.   The  20-ft (6.1  m)  length  was selected on the
basis of the basis weight fluctuation  cycle which the model
paper machine exhibits.  In  addition,  8 minutes prior to -the
taking of the paper  samples, water samples  were collected from
the headbox,  first tray white water  and total wet end overflow.
Water sample  analyses, in conjunction  with  those conducted on
the paper samples, were used to calculate retention values.
                               10

-------
 COATING  TRIAL

      Each  day  three  to  four  30-in.  (0.76 m)  diameter  rolls of
 paper 24 in.  (0.6 m) wide were made.  These  rolls were wrapped
 and shipped to the cooperating company  for coating.   Upon ar-
 rival, the rolls  from each trial were rewound  into large master
 rolls and  trimmed to a  20-in.  (0.5  m) width  for  use on the pilot
 blade coater.   All rolls were coated'using the coating formula-
 tion commercially applied on the simulated grade.  It consisted
 of 100 parts dry weight of clay, and 15 parts  dry weight of  cal-
 cium stearate.  The  pilot blade coater was operated at a speed
 of 1000  fpm  (305 m/min).  The coated paper was supercalendered
 to meet  a  gloss specification of 50 ± 2.  Samples of  the coated
 paper were taken  for testing of the physical and optical proper-
 ties. The rolls  of  paper were then rewound  into two  composite
 rolls containing paper from each of  the  three test conditions.
 These rolls were wrapped and shipped to Rochester Institute  of
 Technology for further  assessment of printing  properties.


 PRINTING TRIAL

      The composite rolls consisted  of a leader of paper manufac-
 tured commercially by the mill, followed by  segments  from each of
 the three  test conditions.   In doing so, the rationale was to get
 the press  set  up  and running on the commercial paper  and then
 print at the same conditions the pilot  paper machine  manufactured
 paper.   The printing was accomplished with a GOSS Commercial
 30-in.  (0.76 m) ,  four-color  perfecting  press equipped with a
 brush dampening system. The four colors run in  sequence were
 cyan (tack 14.2), magenta  (tack 12.0),  yellow  (tack 10.0) and
 black (tack  8.2).  The  press speed  was  controlled at  600 fpm
 (183 m/min), and  the temperature of the web  out  of the drier
 ranged from 200 to 350°F  (93 to 177°C).  There appeared to be
 little difference in the runability of  the different  components
 of the composite  rolls. The printed samples were evaluated  both
 by printing experts  from the cooperating company and  by Dr.  E.W.
 Rayford of Western Michigan  University.  Dr. Rayford's comments
 on the printed samples  are also included in  Appendix  B.  He  was
 asked to evaluate a  series of number-coded samples on ink hold-
 out, strikethrough,  printing smoothness, pick  resistance,  fiber
 rise, sharpness and  showthrough on  a scale of  1  to 5: 1 - poor,
 2 - fair,  3  -  average,  4 - good,  5  - excellent.  Results  can be
 found on Table 6.

 LABORATORY PHYSICAL, OPTICAL AND  PRINTING TESTS

      The paper was evaluated using  methods  commonly practiced in
 the paper  industry.  Following  is a listing  of the various  tests
 performed  and  the method used  for each.  With  the one exception,
 they are either Technical Association  of Pulp  and Paper  Industry
,Standard Methods  (6) or Useful  Methods  (7).

                                11

-------
          Basis Weight

          Caliper

          Tensile

          Stretch

          Sheffield Porosity

          Sheffield Smoothness

          Mullen

          Tear

          Fold

          Brightness

          Opacity

          Gloss

          IGT

          K & N Ink

          Wax Pick

          Dirt Specks

          Hiding Power
                T410

                T411

                T494

                T457

                UM524

                UM518

                T403

                T414

                T511

                T452

                T425

                T480

                T499

                UM553

                T459

                T437

                (described below)
     Hiding power is a control test which is used to monitor
printing showthrough.  The sample of interest is solidly printed
on one side using No. 4 black printing ink  (I.P.I.)  at a con-
stant speed of 0.4 m/sec by means of the IGT printability tester
AC2.  The sample is allowed to dry three hours and the brightness
of the nonprinted side is taken.  The brightness of a nonprinted
sample is also measured, and the corresponding percent reduction
in brightness due to the printing on the opposite side is calcu-
lated as:
        HP = 100(1 -
 Original   _    Opposite Side
Brightness	Printed Brightness,
     Original Brightness
                               12

-------
                           SECTION V

    DISCUSSION OF RESULTS FROM EVALUATION OF SCREENING AS AN

    ALTERNATIVE FOR FILLER RECOVERY FROM HIGH ASH SLUDGE FOR

                   REUSE IN COATED FINE PAPER
SCREENING

     Characteristics of the screening process and the recovered
material is shown in Table 1.  The pilot scale screening trials
conducted at the cooperating mill achieved filler recoveries
(ignition loss compensated ash recoveries)  on the order of 70 to
85 percent; whereas, the laboratory results on a conventional
sludge (nondekining) suggested potential filler recovery of 91.5
percent.  This difference in recovery is probably due to the
difference in composition of the two sludges evaluated.  The
cooperating mill's sludge had a high groundwood content, making
it very hydrous.  Possibly it was harder to separate the fillers
from the hydrous groundwood particles.  The conventional sludge
studied under laboratory conditions did not contain any ground-
wood.  It would follow that the differing composition and proper-
ties of primary clarifier sludges among individual mills would
require screening trials on a site-specific basis to determine
their filler recovery potential.


PHYSICAL AND OPTICAL PROPERTIES OF COATING BASE SHEET

     Table 2 lists the physical and optical properties of the
uncoated base sheet for the three trial conditions.  For compari-
son, the mill-manufactured base sheet properties are also listed.
The column labeled "5% Control" represents simulation of the
mill-manufactured grade.  Comparing these two on a physical and
optical properties basis, one would conclude that they are sig-
nificantly different from one another on many of the properties.

     The column labeled "8% Control" was to simulate the effect
of increasing the ash content to the level of the sheet associ-
ated with reuse of the recovered filler.  A comparison of results
of the 5 and 8 percent virgin filler additions indicates increas-
ing the ash had a negligible effect on the physical and optical
properties.


                                13

-------
      Table 1.  SCREENING CHARACTERISTICS FOR
  FILLER RECOVERY FOR REUSE IN COATED FINE PAPER
           Parameter
    Mill  site  data
Feed consistency  (%)

Feed ash content  (%)

Feed rate  (gpm)/(1/min)

Screen diameter  (in.)/(cm)

Mesh

Recovered  ash  content  (%)

Purity (%)

Total solids recovered  (%)

Filler recovery  (%)

Brightness  (%  elrepho)

Solids loading rate  (lb solids/
   min ft2)/(Kg/minm2)	
            2


         38.2


       2-3/8-11


        30/76


          100


         54.5


         64.1


        50-75


        70-85


         56.7
.07-.!  Ib/min ft  /
  .3-.5 Kq/m2 min
Note:  For comparison, brightness  of No.  2  filler
       clay is  80  to  82.
                          14

-------
           Table 2.   PHYSICAL AND OPTICAL PROPERTIES
                     OF COATING BASE SHEET
Properties
Basis weight ,
(lb/3300 ft2)/(gm/in )
Ash (%)
Caliper (.001 in.) /(mm)
Opacity (TAPPI)
Felt brightness
(% elrepho)
Wire brightness
(% elrepho)
Smoothness (Sheffield)
Porosity (HOP)
MD Tensile (Kg)
CD Tensile (Kg)
Mullen (PSI)/(kPa)
Mullen ply bond (PSI)/
(kPa)
MD Tear (g)
CD Tear (g)
MD Fold (number)
CD Fold (number)
MD Stretch (%)
CD Stretch (%)
MD TEA (KgdrO/m2,)
CD TEA (Kg(m)/nr)
Dirt specks
First pass retention (%)
Overall retention (%)
5%
Control
47.0/69.6

4.4
5.0/0.13
90.3
68.4

68.6

171
120
9.6
5.1
20.7/143
172/1180

62
75
157
25
1.72
3.6
3.4
4.4
554
64.2
79.0
8%
Control
45.2/66.9

8.0
4.8/0.12
89.7
70.4

70.4

171
131
8.3
4.7
16.8/116
168/1160

62
75
111
17
1.71
3.4
2.9
3.8
413
65.4
76.9
Recov-
ered
filler
45.8/67.8

8.6
4.7/0.12
93.3
62~Tja

163. 4la

177
96
8.5
4.4
16.6/114
175/1200

55 a
65 a
84
15
1.74
3.4
3.1
3.7
428
66.0
76.8
Mill
manuf .
base
sheet
46.3/68.5

3.7
4.1/0.10
90.6
72.5

73.4

97
81
11.0
3.9
18.6/128
185/1270

46
62
157
18
1.5
2.4
3.3
2.2
384
—
—
ai	[Significantly lower than 8% control sample
 '	'at 99.5% confidence as indicated by a t te
test.
                               15

-------
     The column designated  "Recovered  filler" reflects the prop-
erties of the  sheet made employing recovered filler to increase
the ash content, thus simulating the way it would be utilized in
the mill.  The best basis for direct comparison with this sheet
is the 8 percent control.   The boxed values in the recovered
filler column  are statistically lower  than the 8 percent control
values.  The apparent small loss in tear is not of practical con-
sequence; however, the drop in brightness of the product is.
The drop of 7.6 points in felt side brightness and 7.0 points in
wire side brightness is of  real concern.  This loss in brightness
caused by the  recovered filler suggested the necessity for
bleaching of the recovered  filler prior to reuse and prompted
the additional investigation of that option, discussed later in
this report.   It should be  noted also  that the brightness of all
of the sheets  made at Western Michigan University are lower than
the products made at the mill.  This was due to the preserved
.groundwood discoloring during storage  prior to
     However,  loss  of brightness was accompanied by the gain of
3.6 points  in  opacity.  The  gain in opacity may be related to the
presence of other filler materials besides clay in the recovered
filler material.  It is interesting to note that the dirt speck
count did not  significantly  increase when utilizing the recovered
filler, although all values  are very high due to the groundwood
content of  the product.

     The first pass and overall retention values, also reported
in Table 2, demonstrate that utilization of recovered filler
does not appear to  have changed the retention characteristics on
the machine.
COATING

     The physical  properties  of  the  coated offset sheets are
summarized  in Table  3.  There does not  appear to be any signifi-
cant deterioration in the physical properties of the sheet due
to either the addition  of the recovered filler or increase in
ash content.  Unlike results  reported for the uncoated sheet, a
difference  in tear between  the sheet containing the recovered
filler and  that  containing  exclusively  virgin filler was not
apparent.   The result reported on the coated sheet was substan-
tiated by additional tests, inclusive of mill testing, and is
felt to be  the^ more  reliable.

     The optical properties of the coated offset sheet are sum-
marized in  Table 4.  The brightness  of  the sheet containing the
recovered filler is  4 points  lower than the 8 percent control,
and its opacity  is 1.8  points higher.   Thus, the loss in bright-
ness of 7.0 to 7.6 points in  the base sheet is dampened in the
coated product.  However, it  remains questionable whether the
                               16

-------
Table 3.  COATED OFFSET SHEET PHYSICAL PROPERTIES
                    Summary
Physical properties
Coat wt (lb/3300 ft2)/
( gm/m2 )
a

Caliper (.001 in) /(mm)

a

MD Tensile (Kg)
a
CD Tensile (Kg)
a „
MD TEA (Kg(m)/nr)
a ~
CD TEA (Kg(m)/m )
a
MC Stretch (%)
a
CD Stretch (%)
a
Porosity (Sheffield)
a
Porosity (HOP)
a
Smoothness (Sheffield)
a
Mullen Q?SI)/(kPa)

a

MD Tear (gm)
a
CD Tear (gm)
a
MD MIT fold (number)
a
CD MIT fold (number)
a
5%
Control
6.15/
9.10
0.10/
0.15
3.79/
0.096
O.ll/
0.003
11.95
0.61
5.91
0.29
4.04
0.53
3.84
0.72
1.75
0.16
2.9
0.38
|28.0|a
0.6
216
22
53.2
7-8
22. 5/
155
2.2/
15.4
57.8
4.2
72.9
3.3
254
83
40.8
11.3
8%
Control
6.17/
9.13
0.13/
0.19
3.73/
0.095
0.13/
0.003
10.0
0.90
5.90
0.23
3.41
0.77
3.97
0.46
1.50
0.22
2.9
0.25
33.8
0.9
204
33
40.1
6.5
19. 6/
135
1.8/
12.5
59.6
3.8
73.8
5.2
184
76
29.1
11.5
Recov-
ered
filler
6. OS/
8.95
0.16/
0.24
3.66/
0.093
0.12/
0.003
11.1
0.46
5.61
0.26
3.31
0.41
4.25
0.46
1.61
0.15
3.3
0.27
31.8
2.3
215
20
48.7
5.6
19. 4/
134
1.8/
12.1
57.7
5.3
69.2
3.7
201
58
26.7
13.0
Mill
manuf .
sheet
6.10/
9.03
0.58/
0.86
3.55/
0.090
O.ll/
0.003
33.9
0.61
5.07
0.32
4.22
0.44
2.77
0.36
1.57
0.10
2.4
0.23
33.9
0.6
182
25
49.7
12.2
20. 1/
138
1.6/
10.7
49.8
6.2
62.0
3.0
186
62
25.2
9.51
Significantly different from recovered  filler sample at
99.5% confidence as indicated by a t test.
                        17

-------
   Table 4.  COATED OFFSET SHEET OPTICAL PROPERTIES
                       Summary
Optical properties
Brightness (% elrepho)
a
Opacity (TAPPI)
0
Gloss (75°)
a
5%
Control
72.2
0.21
94.3
0.31
49.2
5.3
8%
Control
73.3
0.13
94.6
0.29
48.5
2.2
Recovered
filler
|69.3|a
0.22
DEO]*
0.26
47.5
3.2
CPI
73.7
0.16
94.7
0.20
50.6
2.7
      indicates significantly different  from control at
      99.5 confidence level as indicated by a t test.
Table 5.  COATED OFFSET SHEET, LABORATORY PRINTING TESTS
Laboratory printing
tests
IGT Pick (#6 ink)
o
K & N ink (% reduction)
a
Hiding power
a
Fiber rise W/F
B = blisters
(0 = poorest, 4 = best)
285°
255°
230°
5%
Control
92
12.0
19.6
1.3
0.98
0.015
•
1-0
1-0
3-1
8%
Control
88
8.1
20.2
1.5
0.98
0.005

1-0
1-0
3-1
Recovered
filler
88
5.1
20.4
1.9
0.99
0.004

1-0
2-0
3-1
CPI
94
5.5
22.4
3.2
0.97
0.008

1-0
2-1
3-1
                           1 8

-------
mill could, under present marketing conditions, tolerate this
degree of brightness loss.

     The laboratory printing tests for the coated sheet are
given in Table 5, and there appears to be no significant differ-
ence in the laboratory printing properties.   The printing trial
conducted at the Rochester Institute of Technology upon rolls of
coated paper composited from those produced under the various
manufacturing conditions allowed determination under uniform
printing conditions of whether the type of paper affected print
quality.  Four signatures selected at random for each condition
were submitted to a printing specialist for his independent
evaluation.  He was asked to grade each signature on a scale of
1 to 5 for 7 printing properties.  The scale was: 1 - poor,
2 - fair, 3 - average, 4 - good, 5 - excellent.  The printing
properties he was asked to judge were gloss, ink holdout, strike-
through, printing smoothness, pick resistance, fiber rise, ink
spread and showthrough.  The specialist was not aware of the
origin of the samples or purpose of the evaluation until after
the evaluation was completed.  His detailed comments are given in
Appendix B.  The results of his independent evaluations are tab-
ulated in Table 6.

     All three test conditions from the pilot paper machine trial
were rated as essentially identical.  Thus, it appears that the
recovered filler does not affect printability significantly.  The
mill-manufactured paper was graded lower on the properties of ink
holdout, printing smoothness and showthrough but superior in its
lack of fiber puffing.

     Printing experts at the cooperating mill examined the print-
ing quality and reached the similar conclusion that there was
little difference among the three conditions from the pilot trial
at WMU.  However, a difference between these and the commercially
produced paper was cited.  This difference was mostly due to the
color difference between the papers:  the commercial paper was a
more blue-white; whereas, the pilot plant paper had a cream
color.
                                19

-------
                                Table  6 .  COATED OFFSET SHEET  PRINTING RESULTS
Sample
8R
Recov- 8R
ered
Filler 8R
8R
8V
8% 8V
Control
8V
8V
5V
5% 5V
Control
5V
5V
CW
Mill cw
Manufac-
tured cw
Paper
CW-P
(Gloss)
Ink
holdout
4
4
4
2
4
4
3
4
4
4
4
4
3
3
3
2
Strike-
through
4
4
4
4
4
4
4
4
4
4
4
4
4
4
4
4
Printing
(smoothness)
mottle
4
4
4
4
4
4
4
4
4
4
4
4
3
3
3
3
Pick
resis-
tance
4
4
4
4
4
4
4
4
4
4
4
4
4
4
4
4
Fiber
Rise
(puffing)
4
4
4
4
4
4
4
4
4
4
4
4
3
5
5
5
Ink
spread
(sharpness)
4
4
4
4
4
4
4
4
4
4
3
4
3
4
4
2
Show-
through
4
4
4
4
4
4
4
4
4
4
4
4
3
3
3
3
Total
28
28
28
26
28
28
27
28
28
28
27 "
28
23
26
26
24
Aver-
age

27.5


21. IS



21. IS



2^.75


to
o
     1.  Poor
2.  Fair   3.  Average   4.   Good   5.   Excellent

-------
                           SECTION VI

       EVALUATION OF SCREENING AS A RECOVERY ALTERNATIVE

         FOR A MILL MANUFACTURING UNCOATED FINE PAPER
EXPERIMENTAL DESIGN

     A mill selected from its grade structure two grades which
were high volume items and would be likely candidates for plans
to utilize the recovered filler.  It was felt that a heavy grade,
which had a basis weight of 50 lb/3300 ft2 (74 gm/m2), would
probably be able to utilize the recovered filler with little
difficulty.  In addition a 30 lb/3300 ft2 (44 gm/m2)  grade was
chosen as a more critical test of the recovered filler in recog-
nition of long range industry trend toward lighter weight fine
papers.  It was intended that the recovered filler be tested as
a partial replacement for virgin filler clay.  The mill had such
a diverse grade structure, some products of which the recovered
filler would not be suitable for, that no single virgin filler-
recovered filler blend condition emerged as likely to be princi-
pally utilized.  However, practical experimental conditions
suggested that recovered filler clay be added directly to the
beater during the model machine run and that virgin clay be con-
tinuously metered in at a rate necessary to maintain the desired
ash level.  The screening was conducted at the mill site and the
recovered filler shipped to WMU where the two grades were simu-
lated on the pilot paper machine.  The grades were simulated
using virgin filler exclusively and utilizing recovered filler
in combination with virgin clay.  Properties of the paper pro-
duced were evaluated by NCASI personnel.  The rolls produced were
evaluated by NCASI personnel.  The rolls produced were subse-
quently rewound at the cooperating mill before shipment to
Rochester Institute of Technology for printing evaluation on a
four-color commercial web. offset press.
SCREENING PROCEDURE

     The screening was accomplished on site at the cooperating
mill utilizing an unused 30-in.  (0.76 m) Sweco vibrating screen.
Primary sludge at 10 to 12 percent consistency was hauled from
the site of the primary clarifier in half-full 55-gallon (210 I)
drums, diluted at the screen installation to 5 to 6 percent


                               21

-------
using a drum pump and mixed manually.  The screen was equipped
with a 230-mesh stainless steel screen and fed at a rate of 3 to
5 gpm (11.4 to 18.9 £/min).  At the rate of 5 gpm (18.9 A/min),
the screen became flooded and one occasionally had to stop to
allow the screen to clear itself.

     The solids content of the material passing the screen, as
recovered filler, was 3 to 3.5 percent solids and amounted to
approximately 50 percent of the total sludge fed the screen.
Considering only the ash fraction as being the component of
interest, 65 to 67 percent of the total ash or filler was recov-
ered.  The material passing through the screen was 88 percent
filler and only 21 percent organic matter, as calculated from an
ash measurement, compensating for 15 percent ignition loss.  This
material passing through the screen was predominantly filler.

     The screening was conducted over a 1-week period by both
mill and NCASI personnel.  The recovered filler was allowed to
settle, decanted, consolidated to a minimum number of drums and
shipped by truck to WMU.  At the conclusion of each day's
screening and again prior to shipment to WMU, the drums of
recovered filler were treated with 500 ml of formaldehyde to pre-
vent bacterial decomposition.  Upon arrival at WMU, the drums
were all adjusted to 6 percent consistency by addition of city
water and treated with an additional 500 ml of formaldehyde per
drum.
PILOT PAPER MACHINE TRIAL

     The two mill grades simulated during the WMU pilot paper
machine trial were a 30 lb/3300 ft2  (44 gm/m2) Bible-type paper
and a 50-lb (74 gm/m2) offset sheet.  Two days of machine time
were devoted to each grade.  The first day the grade was produced
using virgin filler clay; the second day screened, recovered
filler was substituted for a portion of virgin material.

     The furnish for the 30-lb  (44 gm/m2) sheet consisted of 40
percent Canadian bleached softwood kraft, 20 percent bleached
hardwood kraft, 20 percent semi-bleached softwood kraft and 20
percent broke, which was supplied by the cooperating mill.  The
pulp was refined in the beater to 250 to 300 Canadian Standard
Freeness.  Added to the beater after refining, expressed as per-
cent of O.D. pulp weight, were 5 percent titanium dioxide, 12
percent filler clay and 0.8 percent alum.  In addition, dyes
provided by the cooperating mill were added to tint the paper a
cream color.  The pH was controlled on the machine to 4.8 to
5.0 with sulfuric acid.  The sheet was sized by continuous addi-
tion of Neuphor emulsified rosin size at a rate equal to 2 Ib/ton
of paper (1 Kg/metric ton).  The size was added to a mixing
chamber just prior to the headbox.  The dandy roll was used and


                               22

-------
three nips were used in the calender stack.  The sheet was also
externally starch-sized in the size press.  The starch, Clinton
753B, had been previously batch cooked at 10 percent for use in
the size press.  The size press temperature was held at 140° to
150°F (60 to 66°C), and the pickup rate was about 65 Ib/ton of
product (32 Kg/metric ton).

     The initial headbox temperature selected was 110°F (43°C),
and a retention aid (Dow CP7)  was fed at a rate of 1/2 Ib/ton
(0.25 Kg/metric ton).  These two parameters had to be modified
during the first hour of running the machine due to bad sheet
formation.  The sheet was overflocculated and blotchy, so the
retention aid was stopped and the temperature dropped to approx-
imately 70°F (21°C).  This solved the formation problem.  Addi-
tional filler clay, at 15 percent solids consistency, was metered
into the system to maintain the ash content in the sheet at a
desired 15 percent level.  An additional 9 percent clay was
metered in this manner.  In the absence of a retention aid, the
achievement of such a level in a lightweight grade sheet with
the prescribed furnish on the WMU pilot machine required a 9 per-
cent trim clay addition.

     During the second day of running, recovered filler material
was substituted for the virgin clay added to the beater.  How-
ever, use of virgin filler was continued for the supplemental
trim clay-  The magnitude of trim clay addition was such that
filler materials constituted 57 percent of the clay or 46 percent
of the total filler contained in the 30-lb (44 gm/m^) sheet.
                                       2
     The furnish for the 50-lb (74 gm/m )  sheet consisted of 40
percent southern bleached softwood kraft, 27 percent southern
bleached hardwood kraft and 33 percent broke supplied by the
mill.  The pulp was refined in a beater to 250 to 300 Canadian
Standard Freeness.  Three percent titanium dioxide, 14 percent
filler clay, 0.8 percent alum, expressed as weight of O.D. pulp,
were added after refining; dye also was added and mixed in to
give the sheet a bluish-white cast.

     The pH of the  furnish to the machine was controlled contin-
uously with sulfuric acid to 4.6.  The sheet was internally sized
with Neuphor emulsified rosin size at a level of 2 Ib/ton  (1 Kg/
metric ton), and a retention aid  (Dow CP7) was added to the mix
tank prior to the headbox at a level of 2 Ib/ton  (1 Kg/metric
ton).  Three nips were taken in the calender stack, and the dandy
roll was utilized.  The sheet was externally sized with starch
through use of the  size press, which was operated under condi-
tions similar to those associated with the lightweight sheet.
The starch used was the same as for the 30-lb  (44 gm/irr) grade
and was prepared in a similar manner.  The pickup rate was
approximately 50 Ib/ton of product  (25 Kg/metric ton).  Final
sheet moisture was  controlled to 4 percent.
                               23

-------
     During the first day's run of the 50-lb (74 gm/m2)  sheet no
trim clay was added, but during the second day's run, the ash
level of the sheet was maintained by adding a 15 percent slurry
of filler clay to the mix chamber prior to the headbox.   This
addition represented 2.35 percent of the filler added with the
final sheet ash controlled to 15 percent ± 1.  During the second
day's run on the 50-lb (74 gm/m2) sheet, the filler added in the
beater was replaced by screened, recovered filler.  Thus, during
the run containing the recovered filler, 83 percent of the clay
was recovered filler and 68 percent of the total filler in the
sheet was recovered filler.  A daily sampling routine of collect-
ing four sets of paper and white water samples per day was fol-
lowed similar to that described in the coated fine paper model
machine run.

     The rolls of paper from the four 1-day machine trials were
wrapped and shipped to the cooperating mill, where they were
rewound into four composite rolls, two of which were of the
lightweight grade and two of the heavy-  Each composite roll was
half made with virgin filler and half with recovered filler.
Rewinding problems were encountered with the lightweight paper
which consisted of a series of breaks due to pin holes and dirt
in the paper.  However, these problems were observed in both
sheets made with and without recovered fillers and as a result,
could not be attributed to the presence of reclaimed material.
The composite rolls were then shipped to Rochester Institute of
Technology for printing.


LABORATORY PHYSICAL, OPTICAL AND PRINTING TESTS

     The procedures used are in common practice in the paper
industry and are described in detail in the section on testing
procedures for the coated fine paper evaluation, Section IV of
this report.

PRINTING TRIAL

     The printing was accomplished using a GOSS Commercial 38-
in., four-color perfecting press equipped with a brush-dampening
system.  The four colors used were yellow, magenta, cyan and
black, and they were applied in that order.  The printing speed
was controlled at 520 to 540 fpm  (158 to 165 m/min) and the web
temperature leaving the dryers varied from 220°F to 290°F (104
to 143°C).  The hot air temperature varied from 400°F to 490°F
(204 to 254°C).
                                                           2
     The press was made ready using a roll of 50 lb/3300 ft
(74 gm/m2) mill-manufactured paper.  When the press exhibited
satisfactory printing conditions, it was run for an additional
3000 impressions before a composite roll, consisting of equal
proportions of the 50-lb  (74 gm/m2) control sheet and the 50-lb

                               24

-------
        o
(74 gm/nr)  recovered filler sheet was spliced in and printed.
Two breaks occurred during the rnn of the roll of mi11-manufac-
tured paper and one each during the sections of composite roll
containing the control and recovered filler.

     A roll of 35 lb/3300 ft2 (52 gm/m2)  mill-manufactured paper
was run next as a made-ready roll for printing of a composite
roll of the 30-lb (44 gm/m2) paper manufactured on the pilot
paper machine.  The cooperating mill did not have an extra roll
of the 30-lb (44 gm/m2)  grade which simulated in the pilot trial
so the 35-lb (52 gm/m2)  roll was substituted.  The 35-lb (52 gm/
m2), mill-made paper left a white deposit on the yellow blanket,
and two breaks were experienced during the printing of this roll.
Three breaks occurred in the subsequent printing of the 30-lb
(44 gm/m2)  composite roll, two during the course of running the
section containing only the virgin filler and one during the
segment containing recovered filler.  The second composite roll
of 30-lb (44 gm/m2)  paper was run next, and only one break, dur-
ing the portion containing the recovered filler, was encountered.
                                                         2
     The final roll printed was the second 50-lb (74 gm/m )
basis weight composite roll, and it ran without any breaks.

     The frequency of breaks was undoubtedly detrimental to
quality of the printed sheets.  In the course of the trial, the
occurrence of breaks diminished as the press crew gained experi-
ence in the printing of the grades of paper under study.  Fur-
thermore, to prevent breaks, sheet tension had been progressively
decreased over duration of the trial.

     Each roll or segment of a roll was printed with greater
than 3500 impressions.  Plate wear was observed at the end of
the printing trial after only 60,000 impressions but it is not
possible to say whether this was due to the paper or the stop-
start nature of the press operation.

     After the press had reached steady state, the different
papers printed were sampled every 500th impression by taking 10
signatures.  These signatures were packaged and shipped to
Western Michigan University for evaluation.  From these signa-
tures, five samples from each condition were selected at random
and submitted to an impartial printing expert at Western Michi-
gan University for evaluation based upon seven printing pro-
perties.  These included ink holdout, strikethrough, showthrough,
printing smoothness, ink spread, printing sharpness and pick
resistance.  The samples were judged on a scale of 1 - poor,
2 - fair, 3 - average, 4 - good, 5 - excellent.

     In addition to the samples from each manufacturing condi-
tion, a set of sequential samples were submitted for evaluation
of whether plate wear significantly affected printing sharpness
as the run progressed.

                               25

-------
                          SECTION VII

                     DISCUSSION OP RESULTS


     The cooperating mill in this segment of the study was one
whose sludge had been evaluated in the initial laboratory test
program.  Table 7 is a comparison of the screening results
obtained under laboratory and field conditions.  The purity of
the screened product decreased only slightly, while the percent-
age of the filler which was recovered decreased significantly -
In the laboratory study it was found at a constant solids loading
rate  to the screen that variation in sludge consistency over a
range from 0.1 to 3 percent did not affect the recovery effi-
ciency-  However, it is conceivable that such a trend would not
extend to the 6 percent consistency utilized in the field evalu-
ation.  Going further, a comparison of respective mass loading
rates, expressed as pounds of dry solids/minute per ft2, indi-
cates that the screen under field conditions was loaded at least
an order of magnitude more heavily than under laboratory condi-
tions.  This likely contributed to the lower filler recovery
efficiency and corresponds with the field observation that the
screen at times appeared overloaded and took on a flooded appear-
ance .

     The high feed rate to the screen was chosen under field con-
ditions in order to complete the screening operation in suffi-
cient time to permit the previously scheduled installation of new
equipment by the host mill.  The product recovered, however,
provides a more critical test of the recovered filler's potential
usefulness since it is less pure than the material recovered
under laboratory conditions.

     In the 50-lb (74 gm/m2)  sheet, reclaimed filler materials
constituted 87 percent of the filler clay, which corresponds to
68 percent of the total filler in the sheet.  In the 30-lb  (44
gm/m2) sheet, 57 percent of the filler clay was replaced with
recovered filler, representing 46 percent of the total filler.
The lower percentage of total filler replaced is due to the
addition of titanium dioxide to each sheet.  Its level of addi-
tion was not altered by substitution of filler grade clays with
recovered filler.  The 30-lb (44 gm/m2) sheet contained a higher
percentage of titanium dioxide and exhibited less brightness
loss.
                                26

-------
    Table 7.  COMPARISON  OF LABORATORY SCREENING
VS MILL SITE SCREENING OF CONVENTIONAL HIGH ASH SLUDGE
Parameter
Original sludge ash content (%)
Consistency of feed (%)
Total solids recovered (%)
Filler recovered (%)
Purity of product (% of recov-
ered material which is filler)
Feed rate to screen (gpm)/(l/m)
Screen diameter (in.)/(m)
Screen mesh
Solids loading rate to screen
(Ib solids/min ft2)/Kg/min m2)
Abrasiveness (mg)
Brightness (% elrepho)
Laboratory
data
-
0.1-3.0
-
98
92
0.2 to 4.8/
0.6 to 18.0
18/0.46
230,325
0.023/0.112
-
-
Mill
site
data
55
5-6
50
65-67
88
3 to 5/
11 to 19
30/0.76
230
0.25-0.51/
1.22-2.49
4.2
66.5
                          27

-------
     The first pass and overall retention values experienced dur-
ing the pilot machine runs are summarized in Table 8.  It would
appear from the data that the retention conditions were not sig-
nificantly influenced by the substitution of recovered filler
clay for virgin filler clay in either of the grades simulated.
         Table 8.  UNCOATED OFFSET MODEL MACHINE TRIAL
                        RETENTION VALUES
Sheet produced
2
30-lb (44 gm/m ) control sheet
2
30-lb (44 gm/m ) recovered filler
sheet
2
50-lb (74 gm/m ) control sheet
2
50-lb (74 gm/m ) recovered filler
sheet
First pass ,
29.5
28.3
51.0
54.0
Overall,
67.0
65.0
76.5
77.0
     The physical properties of the sheets made during the pilot
machine run are listed in Table 9 along with the samples of mill-
manufactured paper which were utilized during the printing trial.
In comparing the control sheet to that containing recovered
filler, the figures boxed in the recovered filler column are
statistically significantly different from the control.  However,
none of the differences are of sufficient magnitude to be of
practical concern.  Thus, the use of recovered filler does not
seem to have an adverse effect on the physical properties.  Spe-
cial note should be taken that the dirt speck level of the sheets
containing the recovered filler did not significantly increase.

     The optical properties of the sheets are summarized in
Table 10, and It appears that the brightness is adversely
affected by the addition of the recovered filler.  The 30-lb
(44 gm/m2) sheet lost 0.8 points and the 50-lb  (74 gm/m2) sheet
lost 4.6 points.  The 50-lb  (74 gm/m2) sheet with the recovered
filler gained 1.2 points in opacity.  It is doubtful whether a
mill could tolerate 4.5 points loss in brightness.  As a conse-
quence, if the recovered filler is to be utilized, it would have
to be used in a smaller percentage or would have to be bleached
prior to. use.  Possible techniques for bleaching are discussed
later in this report.

     The laboratory printing test results are summarized in
Table 11.  No differences were noted between the control samples
and samples containing the recovered filler.  In general, the
                                28

-------
                     Table 9.  UNCOATED OFFSET SHEET PHYSICAL PROPERTIES
Test
Basis wt (lb/3300 ft2)/
( gm/m2 )
a

Caliper (.001 in.) /(mm)

a

Porosity (SHeffield)
a
Smoothness (Sheffield)
a
MD Tear (gm)
a
CD Tear (gm)
0
Mullen (PSI)/(kPa)

a

MD Fold (%)
a
CD Fold (%)
a
Paper sample
30-lb
(44 gm/m2)
Control
30. 8/
45.6
0.6/
0.9
2.46/
0.062
0.04/
0.001
161
16
167
11
26.6
3.0
30.4
4.1
11. 5/
79.2
1.5/
10.3
8.1
3.0
5.5
1.5
3U-1JD
(44 gm/m )
Recovered
filler
|29. 7|a /
44.0
0.6/
0.9
|2.35|a/
0.060
0.04/
0.001
147
13
163
8.5
24.4
2.0
31.0
2.0
10. 7/
73.7
1.4/
9.6
7.7
3.5
4.4
0.9
Jb-lD
(52 gm/nr)
Mill
manuf .
35. 6/
52.7
0.3/
0.4
3.19/
0.081
0.07/
0.002
84.5
11.5
168
7.7
37.1
2.1
52.6
4.1
13. 7/
94.4
1.3/
9.0
26.7
8.9
10.8
3.7
50-lb
(74 gm/nr)
Control
50. 6/
74.9
0.3/
0.4
3.80/
0.097
0.05/
0.001
122
13
196
11
67.4
3.3
81.6
5.5
16. 4/
113.0
1.3/
9.0
17.4
4.5
8.2
2.3
t>U-lJD
(74 gm/m2)
Recovered
filler
50. 3/
74.4
0.3/
0.4
3.84/
0.098
0.05/
0.001
| 100|a
7
193
12
66.0
3.0
74.4
3.6
16. 3/
112.3
1.5/
10.3
14.0
3.6
8.3
1.9
i>U-lt»
(74 gm/m2)
Mill
manuf.
58. 8/
87.0
0.21/
0.3
3.88/
0.099
-

94.8
10
220
19
47.4
1.8
54.4
1.6
19. 4/
133.7
3.3/
22.7
7.6
1.8
5.3
1.5
NJ
VD
           Statistically different from the control  at  99.5%  confidence  level  as
           indicated by a t test.

-------
                Table 9.  UNCOATED OFFSET SHEET PHYSICAL PROPERTIES
                                   (Continued)
Test
Sizing (Hercules-sec)
a
Dirt Specks
a
MD Tensile (Kg)
a
CD Tensile (Kg)
o
MD TEA (Kg(m)/m )
a 7
CD TEA (Kg(m)/m )
a
MD Stretch (%)
a
CD Stretch (%)
a
Ash (%)
Paper sample
30-lb
(44 gm/m )
Control
8.9
0.5
5.94
1.9
6.2
0.6
3.17
0.4
1.89
0.4
4.32
0.8
1.5
0.2
4.3
0.5
15.3
30-lb 2
(44 gm/m )
Recovered
filler
10.6
3.0
16.1
7.9
6.3
0.9
3.16
0.3
2.38
0.6
4.32
0.7
1.5
0.2 „
J3TTIa
0.6
15.5
35-lb 2
(52 gm/m )
Mill
manuf.
157
58
25.6
5.8
8.6
0.6
4.3
0.3
1.9
0.4
2.3
0.3
1.0
0.1
1.9
0.2
14.6
50-lb „
(74 gm/m )
Control
95.2
45
11.8
4.2
8.2
0.9
4.4
0.7
6.3
1.2
3.7
0.7
1.8
0.2
4.6
0.8
16.3
50-lb ~
(74 gm/m )
Recovered
filler
83.7
25
12.3
4.3
8.5
0.8
4.2
0.5
6.8
1.8
4.5
1.0
1.9
0.2
4.9
0.8
16.5
50-lb -.
(74 gm/m;
Mill
manuf .
148
36
23.7
8.3
12.9
1.1
4.72
0.2
3.5
0.5
3.09
0.6
0.9
0.1
1.9
0.3
16.4
I	[Statistically different from the control at 99.5% confidence level as
	^indicated by a t test.

-------
                      Table 10.  UNCOATED OFFSET SHEET  OPTICAL  PROPERTIES
Optical
properties
Brightness (G.E.)
a
Opacity (TAPPI)
a
30-lb
(44 gm/m )
Control
78.6
0.25
81.0
1.0
30-lb
(44 gm/m )
Recovered
filler
177.81
0.30
81.4
1.3
35-lb
(52 gm/rn )
Mill
manuf .
77.7
0.22
85.6
1.1
50-lb 9
(74 gm/m )
Control
86.2
0.33
93.1
0.6
50-lb
(74 gm/in )
Recovered
filler
rsTTel a
0.42
194. 3|a
0.6
50-lb
(74 gm/m)
Mill
manuf .
78.3
0.30
91.1
0.5
u>
           Statistically different from control at  99.5  confidence  level  as  indicated
           by a t test.

-------
               Table 11.  UNCOATED OFFSET SHEET  LABORATORY PRINTING PROPERTIES
Test
Wax pick: Wire side
Felt side
Hiding power
a
IGT Pick (cm/sec)
a
Velocity viscosity
product (xlO+ gm/sec )
a
K & N Ink (% reduction)
a
Paper sam
30-lb 2
(44 gm/m )
Control
14
16
76.1
1.3
129.8
20
10.7
1.7
50.8
1.6
30-lb
(44 gm/m )
Recovered
filler
14
16
75.9
2.0
129.3
15
10.6
1.2
53.0
1.7
35-lb -
(52 gm/m )
Mill
manuf .
10
20
89.4
0.2
115.0
7.9
9.5
0.6
52.9
2.0
pie
50-lb
(74 gm/m )
Control
14
14
91.9
0.4
100.9
11
8.3
0.9
54.2
1.0
50-lb
(74 gm/ni )
Recovered
filler
14
14
93.0
0.7
106.5
8.5
8.8
0.72
53.3
0.9
50-lb
(74 gm/m )
Mill
manuf.
16
11
95.1
-
129.0
14
10.6
1.2
55.0
2.1
U)
to

-------
breaks previously cited hampered the printing with the conse-
quence that overall printing quality achieved was not very good.

     Though the printing expert was unaware of which samples
were associated with which grades of paper, it was obviously
easy to distinguish the heavy basis weight sheets.  His detailed
comments are given in Appendix C.  Table 12 summarizes the re-
sults of his evaluation.  Each trial condition had five signa-
tures evaluated.  For the 50-lb  (74 gm/m2) grade, the sheets con-
taining recovered filler were judged superior to the control on
ink holdout, strikethrough, and printing sharpness.  It compared
very well to the mill-manufactured paper.  For the 30-lb (44 gm/
m2) grade, the sheet containing the recovered filler rated poorer
than the control on printing smoothness and sharpness but they
differ by only 1 point in their overall rating.  Both the control
and the sheet containing the recovered filler rated below the
mill-manufactured paper but this was probably due more to the
basis weight difference between the 30- and 35-lb (44 and 52 gm/
m2) sheets than to any other factor.

     Considering all of the printing results as a whole, it would
appear that the recovered filler addition was not a prime factor
in affecting printing properties.  It was the opinion of the
printing expert that varying press conditions were the prime
factor, even though the trial design was set up to minimize this.

     During the printing trial, plate wear was observed and to
see if this significnatly influenced the printing characteris-
tics, a set of sequential samples arranged in the order in which
the printing was done was submitted to the printing expert for
evaluation.  These samples consisted of an early signature and a
late signature from the printing of each individual paper condi-
tion.  From an examination of the results shown in Table 13, it
is apparent that although the printing sharpness did vary
throughout the run, there is not a trend to relate it to plate
wear.
                                33

-------
Table 12.  EVALUATION OF WEB OFFSET PRINTED SAMPLES





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rH g 0) rH
1 & > rH
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in ^f o m
— »p^ Aver
CN
grH
iQ ^^ O
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^^ c!
m ^* O"
r- u _
^> Avg
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-* Avg
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H
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,cj

^
cj
M
4
4
4
3
4
3.8
4
4
4
4
3
3.8
3
3
3
3
3
3
3
3
2
2
3
2.6
1
1
1
1
1
1
1
1
1
1

1




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3
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4
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2.2 4
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3.8
3
3
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2.8
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3 i 2
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2
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2.6
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1
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1
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1
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1
2
3
2.0
1
1
1
1
1
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1
1
4
4
4
4
4
4
4
4
4
4
4
4
4
3
4
3
2
3.2
4
3
2
3
4
3.2
4
3
3
4

4
3.6
j^
p.
CO

^
G
i— i
4
4
4
4
5
4.2
4
3-4
4
4
4
4
3
4
3
4
2-3
3.4
4
4
4
3
3
3.6
3
4
3
3
4
3.4
4
4
4
3

2
3.4


CQ
cn en
G 0)
•H (3
•P Pu
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Lt. ink 4
Lt. ink 4
Lt. ink 4
Lt . ink 4
Lt. ink 4
4
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4
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EH (tl


27.0





28.2





23.6




21.2





16.6


5
5
5
5
2 5
17.6


2 | 5
2.6 5


Grading Scale:
            1 - poor, 2 - fair, 3 - average, 4 - good
            5 - excellent
                         34

-------
Table 13.  PRINTING SHARPNESS
     OF SEQUENTIAL SAMPLES
Sample
Number
Al
A2
Bl
B2
Cl
C2
Dl
D2
El
E2
PI
P2
Gl
G2
HI
H2
11
12
Jl
J2
Kl
K2
High-
lights
3
4
4
3
1
2
1
2
2
3
1
2
1
1
2
2
2
1
1
2
3
3
Middle-
tones
1
4
3
2
2
2
1
1
3
3
1
3
1
1
1
1
1
2
1
3
2
3
Shadow
areas
1
4
3
2
1
3
1
1
2
2
1
2
1.
2
1
1
2
2
1
2
2
2
Average
2
4
3-4
2-3
1
2-3
1
1
2
2
1
2
1
1
2
1-2
2
2
1
2-3
2
3
Grading scale:
   1 - poor, 2 - fair, 3 - average,
   4 - good, 5 - excellent
               35

-------
                          SECTION VIII

            BLEACHING OF SCREENED, RECOVERED FILLER


     The chief drawback to the use of the screened, recovered
filler appears to be its low brightness.  This phenomena was
observed in all three grades of paper manufactured incorporating
the screened, recovered filler.  There are a variety of bleaching
techniques which might be of value in restoring the brightness
of the recovered filler.  Sodium hydrosulfite is commonly used in
the clay industry to bleach its clays.  As a result, it was eval-
uated over a variety of conditions on the screened sludge used
in the manufacture of the uncoated offset sheets.  The tempera-
ture was varied from 150 to 200°F (66 to 93°C).  The concentra-
tion of Na2$204 was varied from 5 to 20 percent, and the EDTA
level from 0.5 to 2 percent.  The best condition appeared to be
1 percent EDTA and 15 percent sodium hydrosulfite for 1 hour at
180°F (82°C), but this resulted in only a 3-point gain in bright-
ness .  This 3-point gain would only increase the brightness from
70 to 73 and probably would not be enough to overcome the degra-
dation of final sheet brightness.

     A variety of other bleaching techniques common to the paper
industry were also evaluated under severe bleaching conditions
on two high ash sludges from conventional mills which were not
deinking.  These techniques included borohydride, chlorination,
hypochlorite, chlorine-water system at pH 5, chlorine dioxide
and peroxide.  The bleaching conditions are summarized in Table
14, and the results given in Table 15.  It appears that all of
the oxidative techniques have the ability to brighten the sludge,
with peroxide showing the greatest capacity-  Thus, bleaching
may provide an alternative to the brightness loss difficulty.
Economic comparison of the various options warrants further
evaluation.
                               36

-------
                             Table.  14.   CONDITIONS FOR BLEACHING
Experimental
parameters
Consistency
PH
Time
Temperature
% Chemical


Additional chem-
ical
Post treatment
Types of Bleaching
Boro-
hydride
2% SS
10
100 min
room
2




Chlori-
nation
2% SS
1-2
1 hr
room
6.59% avCl



Thiosul-
fate
Hypo-
chlorite
2% SS
11-12
2 hrs
room
10% avCl



Thiosul-
fate
CK>2
2% SS
3.5-6.0
5 hrs
160°F(71°C)
1.2



Thiosul-
fate
Chlorine -
H20 pH 5
2% SS
5
1 hr
room
10% avCl



Thiosul-
fate
Peroxide
2% SS
10-11
1 hr
160°F(71°C)
1.5% of
100% chem-
ical
5% Na2Si03
1% Mg SO4
S02 wash
U)

-------
          Table 15.  BLEACHING RESULTS
Type
of
bleaching
No bleaching
Borohydride
Chlorination
Hypochlorite
Chlorine - H20 pH 5
Chlorine Doxide
Peroxide
Brightness, % Elrepho
A
Sludge
70.5
70.0
74.2
75.9
77.5
76.8
77.3
B
Sludge
50.0
52.0
67.4
56.2
64.4
55.6
70.9
Note:
Sludge A originated at the same mill
from which sludges used in the uncoated
fine paper evaluation were taken.

Sludge B originated at a small fine
paper/specialty mill.  Originally low
brightness of the sludge is attribut-
able to excessive clarifier residence
time.
                        38

-------
                           SECTION IX

          PLAUSIBLE SCREENING SYSTEM TO RECOVER FILLER


     If a mill were to employ screening to recover filler from
their high ash sludge as a sludge volume reduction technique,
the flow schematic might be the one shown in Figure 2.   The pri-
mary clarifier underflow is fed through a consistency regulator
to a screening device.  Sludge components which pass the screen
are sent to a mix tank with sufficient residence time to dampen
recovered filler quality variations.  The mix tank might also
function as a tank in which to do any bleaching, if necessary.
From the mix tank the material would flow to the mill for addi-
tion at the usual point where filler is added in the system,
such as a blend chest.

     There are many facets in designing a filler recovery system
to which the previously discussed trials and data do not speak.
However, if one were to make recommendations from the data con-
tained in this report, as far as the consistency fed the screen,
about 3 percent would be a good figure on which to control.

     As far as screen types are concerned, the Sweco vibrating
screens which were used in these studies worked well, but there
are other alternatives commercially available which might be
considered.  A trial was attempted using the Sweco concentrator
rather than their normal flat vibrating screen and it gave very
poor recovery efficiencies when tested.  The screen retained most
of the filler as well as the fiber.

     The mesh of the screen to be employed depends on how much
contamination the grades run can tolerate.  A 320-mesh screen
gives a very pure product.  Employing a more open mesh would
result in more contamination but a greater throughput rate and
associated reduction in required screening surface area.  Life
of the screen is a factor of consideration as well.

     Explicit size and design criteria for the equalization
chamber is elusive.  Equalization required would be dependent
upon the mill's grade structure and frequency of grade changes.
The more changes and wider the variety, the longer will have to
be the equalization chamber to dampen these out.
                               39

-------
              PRIMARY

              CLARIFIER
>£>
O
                                                   MATERIAL RETAINED
                                                   TO  DISPOSAL
SCREEN-
  ING
DEVICE
                                                       MATERIAL
                                                       PASSING
                                                         THE
                                                       SCREEN
                                  WATER
                                                                                   CO
                                                                                 0:1-
                                                                                 LUZ
                                                                                 _)•-«
                                                                                 -10
                                                                                 M Q_
                                                                                 -10
                                     Q
                                    O Q
                                                                 EQUALIZATION CHAMBER
                                                                 AND/OR BLEACHING
                                                                 CHAMBER
              Figure  2.   Diagram of possible scheme for mill installation.

-------
     For" a small specialties mill, the screening of the primary
clarifier sludge might not be the route to follow.  There it
would likely be preferable to go back into the mill, catch the
losses close to the point of origin, and reuse them immediately -
For example, one source of filler loss to the sewer is from the
cleaner rejects.  One specialty mill is currently using 325-mesh
Sweco vibrating screen to recover the filler from this source by
taking the material passing through the screen and sending it
back to the headbox fan pump (8).  No adverse effect on product
quality has been observed.  However, it is important not to send
the screen accepts back to the primary cleaner intake.  Other-
wise, the cleaner system will be overloaded with filler.  This
scheme has a particularly -good return on investment where Ti02 is
being used as filler.  It is a good illustration of isolating the
loss at the source point and immediately reusing it.


MILL EXPERIENCES INCORPORATING PRIMARY CLARIFIER HIGH ASH
SLUDGE INTO A BLEACHING SEQUENCE

Case I (9)

     A fine paper mill producing 485 tpd (440 metric tpd)  of a
mix of bond, offset, book publishing and reprographic papers,
when confronted with the 1974 pulp shortage, decided to reacti-
vate a portion of a dormant three-stage bleach plant to process
100 tpd (91 metric tpd) of semi-bleached hardwood pulp which had
been manufactured at another location.  The pulp would be
bleached in a hypochlorite stage to achieve an 84 to 86 bright-
ness .  At this same time it was decided to reclaim the 10 tpd
(9.1 metric tpd) of primary clarifier sludge which the mill
produced by blending it with the semi-bleached pulp prior to the
thickener preceding the hypochlorite stage.  The bleaching con-
ditions used in the hypochlorite stage were 10 percent stock con-
sistency, 2-hour detention time, calcium hypochlorite to give
3 percent available chlorine, 0.5 percent sulfamic acid, 120°F
(49°C) and pH 7 to 8.  These bleaching conditions worked fine on
the pulp alone, but on the sludge pulp combination it was found
to give a brightness of less than 80 G.E.  Upon investigation in
the laboratory it was found that the primary clarifier sludge by
itself could not be bleached above 55 G.E. brightness.  A strict
blending of 10 tons (9.1 metric tons) of 55 brightness sludge
with 100 tpd (91 metric tpd) of 85 brightness pulp should give
an 82 brightness product which would have been acceptable, but
this additive relationship did not hold, and it was found exper-
imentally that only 5 tpd (4.5 metric tpd) of sludge could be
utilized if the brightness level were to be maintained.

     A second difficulty with the sludge was that the ash frac-
tion was retained poorly on the thickener so a fair portion of it
returned via the thickener filtrate overflow to the clarifier,
thus producing a dead load in the loop between the thickener

                               41

-------
and the clarifier.  A third difficulty which the sludge caused
was plugging of the centricleaners which followed the hypochlor-
ite stage.  After the hypochlorite stage, the stock is diluted
to 1 percent, sent through three stages of centricleaners,
pumped to a vacuum washer and then pumped to the paper mill.  The
rejects from the third stage centricleaners are sent over a Bauer
Hydrasieve and trucked to a land fill.  This acts as the purge of
material from the system.  The filtrate from the hydrasieve was
sent back to the clarifier.  The mill lived with the above diffi-
culties and utilized about half of its primary clarifier sludge
from July through November of 1974.  At this time the operations
were suspended because the extra bleached pulp capacity was not
needed.

     After this experience an economic analysis indicated that
it would be advantageous to continue recovery of the clarifier
sludge even if fully bleached pulp or broke were used as a car-
rier instead of semibleached pulp.  It must be kept in mind that
there were no capital investment costs, only operating costs of
utilizing existing equipment which was available in the inactive
bleach plant.

     Before pursuing this, however, efforts were made to trace
down and alleviate some of the problem areas.  The primary clari-
fier was fed by total mill effluent, storm sewers, roof drains,
septic tank leachings, boiler house sewers, and backwash from
the water treatment plant sand filters.  By daily monitoring of
laboratory bleached brightness of the clarifier sludge, it was
observed that when storm runoff was present, poor brightness of
the bleached sludge resulted.  When the intake water was very
turbid, a lot of filter backwash was in the primary clarifier
sludge and this caused lower brightness.  This amounted to 1 ton
(0.9 metric ton) of silt in 10 tons (9.1 metric tons) of sludge
where normally there would be 500 Ibs (227 Kg) of filter back-
wash in 10 tons (9.1 metric tons) of sludge.  The mill negotiated
with the state for permission to place the filter backwash back
in the water intake basin, and this feed stream was taken out of
the primary clarifier.  This resulted in an average increase of
10 G.E. points in sludge bleachability moving from an average
of 55 to an average of 65.

     The storm sewer runoff was still a problem, but it was
determined that it would be a problem only 25 percent of the time
and moving the coal piles and rerouting storm runoffs so they
would not drain to the clarifier would bring this sufficiently
under control.

     Laboratory studies showed that addition of a chelating
agent before bleaching could increase the brightness an addi-
tional 3 points.  In practice it would be too costly to do this
on a full scale, but it was felt that perhaps iron in the boiler
                               42

-------
blow-down water was the source of this and an alternate way to
dispose of this stream is being sought.

     To solve the loss of filler on the first washer it was
decided to apply the sludge through a drilled pipe to the surface
of the washer after the pulp mat was formed.  This brought the
solids loss problem under control.

     To solve the centricleaner plugging problem it was thought
that placing an 1/8-in. (0.32 cm) opening vibrating-type Johnson
screen prior to the clarifier sludge surge tank and placing a
pressure-type centriscreen prior to the centricleaners would
alleviate this problem.  These are possible future refinements
of their existing system.

     The sludge bleaching recovery system illustrated in Figure
3 was operated for most of the month of June.  Forty tpd (36.4
metric tpd) of fully bleached pulp was fed to a thickener prior
to the hypochlorite retention tower.  This thickener had been
the caustic washer of the inactive bleach plant.  Ten tpd (9.1
metric tpd) of sludge were fed into the chlorination tower of
the inactive bleach plant and treated with calcium hypochlorite
to a level of 3 percent available chlorine.  The chlorination
tower was run as a short retention, completely mixed system at
ambient temperature.  The sludge was fed through showers to the
face of the caustic washer and then into the hypochlorite tower
with the pulp.  Calcium hypochlorite, to give 0.5 percent avail-
able chlorine on the pulp, was added to the hypochlorite tower.
The stock consistency in the tower was 10 percent; 4 hours de-
tention time was utilized at a 120°F (49°C) temperature and a
pH of 7 to 8.

     The stock-sludge mixture was diluted with papermill white
water and sent to the centricleaners.  After the centricleaners,
it was thickened on a vacuum washer and sent to the paper mill
for utilization.  The centricleaners still had plugging problems
but the solids loss problem and the brightness problem were
brought under control.  The sludge processed in this fashion did
not appear to cause any problems when utilized in the mill.
Further modification of the system to include screening devices
to solve the centricleaner plugging problem is anticipated.

     This system or some alternate scheme will be in use in the
near future at this mill to recover their primary clarifier
sludge.

Case II  (10)

     A pulp and paper mill producing 500 tpd  (455 metric tpd)
of fine paper  (book, bond, offset, ledger, duplicator, repro-
graphic, etc.) and 650 tpd  (590 metric tpd) of bleached soda
pulp is reusing its primary clarifier sludge by sending it back

                               43

-------
        CLARIFIER
     REJECTS TO
      LAND FILL
                                      VIBRATING
                                       SCEEE1
                                                                      \[
                                                                           CaOC*
                                                                 /STOCK
                                                                4   *
V/YYYYYY-YYYTrrv
^
S
/
10% SLURRY
f
                                                                CaOCfc
                                                              RETENTION
                                                              V, TOWER
                                                                   ^
                                                                                     CAUSTIC
                                                                                      TOWER
                                                                                     BLEACHED STOCK
                                                                                     CAUSTIC WASHER
                         FILTRATE
                                                                                   SEWER
TO MILL
       SEWER
PAPER MACHINE
 WHITE WATER
 Figure 3.   Case I  primary  clarifier sludge utilization bleaching system.

-------
through the bleach plant.  This mill has a separate sewer system
for the pulp mill and bleach plant areas.  The sewer stream,
whose solids are reclaimed, consists of the papermill sewer, wet
lap machine sewer, storm sewer.- and flexographic printing opera-
tion sewer.  These streams are fed through a 1/2-in. (1.3 cm)  bar
screen, to a 1/8-in. (0.32 cm) bar screen and then into a 60-mesh
sidehill screen, which reclaims much of the pulp solids.  The
filtrate passing the screen is sent to two highly over-loaded
settling primary clarifiers, whose overflow goes to the city
sewage treatment plant.  The clarifier underflow is combined with
the solids recovered from the sidehill screen and sent to a
chest where they are blended with mill colored broke.  The com-
bined clarifier underflow and sidehill screen accepts consist
of approximately 50 percent ash which contains titanium dioxide,
talc, clay, and hydrated silica.  This blend is then shipped to
the brown stock surge tank prior to the chlorination stage.  The
approximate proportion of material processed through the CEHD
bleach plant is 600 tpd  (546 metric tpd) virgin pulp, 15 tpd
(13.6 metric tpd)  clarifier and sidehill screen sludge and 10 tpd
(9.1 metric tpd) colored broke.  The approximate bleaching con-
ditions employed are given in Table 16.  No overt change in the
bleaching chemical demand was noticed when the clarifier sludge
was introduced.  The mill had been reclaiming the sidehill
screen-captured material for approximately 20 years and has been
utilizing the clarifier underflow  in this manner for a year and
a half.

     The only problem which has been noted is an increase in the
dirt count in the final paper product during periods of heavy
rainfall.  Most of the dirt is usually taken out in the Radiclone
system in the bleach plant, but in heavy rainfall periods this
purge is insufficient.  The stock out of the bleach plant is used
to manufacture all of the grades commonly produced by the mill.
The only grade in which it caused difficulty was a perforator
base paper grade which had a low ash requirement.  Since ash was
already present in the pulp coming from the bleach plant, virgin
pulp had to be substituted.
                               45

-------
                     Table 16.  BLEACHING CONDITIONS FOR MILL RECLAIMING
                     CLARIFIER SLUDGE BY PROCESSING THROUGH BLEACH  PLANT
Conditions
Detention time (min)
Consistency (%)
Temperature (°F)/(C°)
PH
Chemical (wt % Of
O.D. pulp)
C
27
3
90/32
2.0-2.5
3% avg cS,
C*,2
E
17.1
8
140-150/60-66
10.0-11.0
1% '
NaOH
H
81.5
8
120/49
8.5-9.5
3% avg cH
CaOCJl
D
326
8
160/71
3.0-3.5
0.5% avg cH
cao2
OS
      635 tpd (580 metric tpd) through plant

-------
                           SECTION X

         EVALUATION OF FILLER RECOVERED BY WET OXIDATION
EXPERIMENTAL DESIGN

     The overall experimental design involved the cooperating
fine paper mill practicing deinking, picking from its grade
structure a high volume 50 lb/3300 ft2 (74 gm/m2) uncoated offset
sheet which was to be simulated on the pilot paper machine at
Western Michigan University-  This grade was to be manufactured
using virgin filler material and then made with the filler com-
pletely replaced with wet oxidized, recovered filler.  The wet
oxidized, recovered filler was obtained by the mill's having
shipped drums of their dewatered clarifier sludge to a commercial
wet oxidation equipment supplier (Zimpro, Inc.)  for processing.
The paper produced was tested for its physical and optical prop-
erties, rewound at the cooperating mill, and shipped to a nearby
commercial printer for a printing evaluation.


WET OXIDATION PROCEDURE

     Dewatered primary clarifier sludge was placed in 55-gallon
(210 H) drums by the cooperating mill and shipped to Zimpro, Inc.
in Rothschild, Wisconsin for wet oxidation.  The material was
reslurried and processed through their pilot plant at a tempera-
ture of 600°F (316°C) and a retention time of one hour.  This
resulted in a pressure in the reaction chamber of approximately
3000 psi (21000 kPa).  The solids fraction, after being wet
oxidized, appeared very similar to virgin filler.  The liquid
fraction had a distinct yellowish tint to it.  As a result, the
solids fraction was washed by allowing it to settle, decanting
the liquid and reslurrying in tap water.  This process was re-
peated several times to ensure removal of the yellow supernatant.
The material was concentrated to 15 percent solids and shipped
to Western Michigan University in plastic-lined, 55-gallon  (210 £)
drums.

     The wet oxidation condition of one hour at 600°F  (316°C) is
as severe an oxidation condition as the processor had ever
observed.  At the time of the trial, they had developed experi-
ence with high ash sludges from five different plants.  To ob-
tain a satisfactory high-brightness product the temperature


                               47

-------
conditions generally ranged from 482°F to 600°F (250°C to 316°C).
The conditions needed to achieve a satisfactory product is some-
thing which will have to be determined on each individual sludge.
Again, the sludge utilized in this study was the most difficult
case that had been encountered, requiring the most intensive of
conditions to achieve high brightness.


PILOT PAPER MACHINE TRIALS

     The pilot paper machine at Western Michigan University was
utilized to make a 50 lb/3300 ft2 (74 gm/m2) sheet from a furnish
consisting of 40 percent bleached softwood kraft and 60 percent
bleached hardwood kraft refined to 300 Canadian Standard Freeness
with a Claflin refiner.

     The sheet was filled to a level.of 15 percent ash using
No. 2 coating clay on the first day of a 2-day trial, and wet
oxidized, recovered filler on the second day.  The sheet was
rosin sized at a level of rosin addition of 8 Ib/ton (4 Kg/metric
ton) and alum addition of 10 Ib/ton  (5 Kg/metric ton) .  The pH
on the machine was kept at 4.5 using sulfuric acid.

     The headbox temperature was kept at 110°F (43°C) and a re-
tention aid, Kato 15 cationic starch, was metered in at a mix
tank prior to the headbox at a level of 10 Ib/ton (5 Kg/metric
ton).  The dandy roll was run on the machine and three nips were
taken in the calender stack.

     The sheet was sized externally by use of the size press.
Penford 280 ethylated starch was used at 6 to 7 percent solids
and the size press temperature kept at 140°F (60°C).

     The machine was run 7 hours manufacturing paper for the
control sample which contained the No. 2 coating clay as filler
and 6 hours manufacturing paper for the wet oxidized, recovered
filler sheet.

     When starting to run the recovered filler sheet, problems
were encountered with pH control on the machine.  The acid
strength had to be increased several  fold in order to compensate
for the demand imposed by the wet oxidized, recovered filler.
This will be explained further in the discussion of results.

     During each day's run, four 30-ft (9.1 m) lengths of paper
were.taken for later evaluation.  Samples of the headbox, first
tray water, and wet end overflow were taken also in order to
establish retention characteristics.
                               48

-------
PRINTING TRIAL

     The printing trial was conducted at Banta Corporation in
Neenah, Wisconsin.  An American Type Founders, four-color, blan-
ket-to-blanket, perfecting offset press was utilized.   The color
sequence used was blue, red, yellow, black.  The paper surface
temperature was kept at 190°F (88°C) after the dryers.  The
printing speed was 700 to 800 fpm (215 to 245 m/min).   The press
had a cloth dampening system.

     The test paper was printed at the end of a regular commer-
cial run.  The plates had 23,000 impressions on them at the start
of the trial.  A roll of the control paper was printed with about
2500 signatures.  A roll of paper containing the wet oxidized,
recovered filler was subsequently printed with approximately the
same number of signatures.  One hundred signatures were randomly
collected from each roll and shipped back to Western Michigan
Unviersity for evaluation.  From these 200 signatures, 5 from
each condition were randomly selected and submitted to a printing
expert for evaluation of 5 printing properties:  holdout, strike-
through, showthrough, smoothness and sharpness.  They were eval-
uated on a scale of 1 - poor, 2 - fair, 3 - average, 4 - good,
5 - excellent.
LABORATORY PHYSICAL, OPTICAL AND PRINTING TESTS

     The same set of tests were used as were discussed in
Section IV of this report.
                               49

-------
                            SECTION XI

                 DISCUSSION OF RESULTS FOR USE  OF

        WET OXIDIZED,  RECOVERED FILLER AS A FILLER PIGMENT


      The  wet oxidized,  recovered filler appears  and  acts very
much  like a normal clay slurry.   Characteristics are shown in
Table 17.  It was handled and metered during the pilot machine
trials in the same manner as  a clay slurry.  The only difficulty
which arose was  with  pH control on the machine.   pH  control
proved impossible until the acid strength was  increased several
fold.   To check  the magnitude of this acid demand, as compared
to  a  sample of No. 2  coating  clay, a 25 ml sample of wet oxidized
recovered filler slurry was titrated with .IN  sulfuric acid  from
its pH of 7 to the pH 4.5 used in the pilot machine  trials.  From
Figure 4  it is apparent that  the recovered filler consumes about
48  times  as much acid as normal No.  2 coating  clay.   This calcu-
lates  out to 2.73 x 10    equivalents of acid/gm  of wet oxidized,
recovered filler.   The  acid demand of the wet  oxidized, recovered
filler at pH 4.5 will be an additional cost to be born.  This
problem can be avoided  by running at neutral conditions.  The
increased  acid  demand  may have been due to calcium  carbonate
being present in the  wet oxidized, recovered filler.


        Table 17.   CHARACTERISTICS OF FILLER RECOVERED BY
                 WET OXIDATION OF DEINKING SLUDGE
Parameter
Original sludge ash content (%)
Oxidized sludge ash content (%)
Oxidized sludge purity (%)
Brightness (% elrepho)
Abrasion (mg)
Pilot data
45.0
85.0
100.0
81.4
6.4
     Table 18 gives the retention characteristics for each day of
the pilot machine run.  There does not appear to be a significant
difference in the retention behavior of the wet oxidized, recov-
ered filler as compared to No. 2 coating clay.
                               50

-------
                      NO, 2 COATING CLAY
                              WET  OXIDIZED



                                FILLER
Figure 4.  Acid demand of wet oxidized pigment.
                     51

-------
            Table 18.  RETENTION CHARACTERISTICS OF
                 WET OXIDIZED RECOVERED FILLER
Control sheet
Wet oxidized recovered
filler sheet
First pass
73.1
74.4
Overall
83.6
84.8
     The physical properties of the sheets made during the pilot
trial and a sample of the mill-manufactured paper which was being
simulated are given in Table 19.  Only MD TEA was significantly
different from the control at the 99.5 confidence level and is
not far enough out of line to be of practical concern.  Note
also that the dirt count did not increase significantly.

     The optical properties of the sheets are listed in Table 20.
The sheet containing recovered filler lost 2.6 points in bright-
ness but gained  4.9 points in opacity-  This kind of a trade of
opacity for brightness could probably be tolerated.  The increase
in opacity may be due to the presence of titanium dioxide in the
recovered filler; whereas, there was none at all present in the
control sheet.  Analysis of the wet oxidized, recovered filler
showed it to contain about 1 percent Ti02 which would account
for about half of the opacity increase.

     The laboratory printing properties are given in Table 21.
The only difference between the control sheet and the sheet con-
taining the recovered filler is in the test for hiding power
where the increased opacity of the sheet containing the recovered
filler manifests itself.

     The paper was shipped to a commercial printer and printed on
a four-color ATF perfecting web offset press.  One roll of paper
containing the wet oxidized, recovered filler was run as was a
roll of the control.  The results of the printing evaluation are
presented in Table 22.  The print quality was very uniform and
the wet oxidized pigment sheet compared well to the control
sheet, rating better than the control on showthrough.  The
printing expert's detailed comments are contained in Appendix D.
                              -  52

-------
Table 19.  WET OXIDIZED, RECOVERED FILLER UNCOATED
         OFFSET PAPER PHYSICAL PROPERTIES
1
Physical properties
Basis weight (lb/3300 ft2)/
( gm/m2 )
a
Caliper (.001 in) /(mm)
a
Porosity (Sheffield)
a
Smoothness (Sheffield)
a
MD Tensile (Kg)
a
CD Tensile (Kg)
a
MD Tensile factor
a
CD Tensile factor
a
MD Stretch (%)
a
CD Stretch (%)
a
MD TEA (Kg(m)/m )
a ~
CD TEA (Kg (m) /m )
a
Mullen (PSI)/(kPa)
a
MD Tear (gm)
a
CD Tear (gm)
a
MD MIT fold (number)
a
CD MIT fold (number)
a
Dirt specks
a
Control
51.8/76.7

1.1/1.6
3.80/0.097
0.0 /0.002
117
3.1
125
15.2
10.0
0.35
5.65
0.30
0.13
0.005
0.073
0.004
1.82
0.15
3.79
0.59
3.55
0.36
5.02
1.1
18.3/126
1.5/10.3
58.4
5.6
63.5
4.2
62.9
35.1
21.5
6.4
45.0
Recovered
filler
51.4/76.1

1.1/1/6
3.85/0.098
0.10/0.003
115
6.7
121
21.2
9.16
0.62
5.38
0.22
0.12
0.009
0.070
0.003
1.63
0.14
4.10
0.47
|2.88| a
0.38
5.24
0.73
17.4/120
0.95/6.5
59.3
4.0
67.9
5.1
60.2
17.1
18.9
4.6
58.8
13.4 9.1
Mill
Made
46.5/68/8

1.4/2.1
3.55/0.090
0.05/0.001
102
6.1
153
27.8
9.39
0.79
6.23
0.28
0.136
0.008
0.09
0.004
1.64
0.18
4.23
0.46
2.94
0.49
6.32
0.95
20.5/141
2.1/14.5
48.4
3.4
49.0
4.3
100.4
27.5
63.8
15.7
—
—
 Statistically different from the control at 99.5%
 confidence level as indicated by a t test.
                         53

-------
  Table 20.   WET OXIDIZED, RECOVERED FILLER
  UNCOATED OFFSET PAPER OPTICAL PROPERTIES
Optical properties
Brightness
a
Opacity (TAPPI)
a
Units
% Elrepho
Control
82.5
0.15
85.4
0.52
Recovered
filler
(HIl]a
0.17
[9073] a
0.59
Mill
Made
77.7
0.39
89.6
0.45
  Statistically different from control at 99.5
  confidence level as indicated by a t test.
 Table 21.  WET OXIDIZED, RECOVERED FILLER
UNCOATED OFFSET PAPER PRINTING PROPERTIES
Lab printing properties
Wax pick
a
K & N Ink
a
Hiding power
a
WP (x 10 4) gm/sec2
a (x lO*)
Hercules size (sec)
a
IGT Pick (cm/sec)
(Polybutene oil 822 poise) a
Control
12.1
0.45
48.4
4.25
0.87
0.028
9.7
0.82
58.6
21.2
118
10.9
Recovered
filler
11.1
0.80
52.3
5.09
|0.93a
0.007
10.0
1.17
77.6
10.9
122
14.0
Mill
made
13.2
0.83
44.4
6.48
0.90
0.014
21.7
2.1
76.7
15.2
264
26
 Statistically different from control at 99.5
 confidence level as indicated by a t test.
                      54

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                       Table 22.   UNCOATED OFFSET SHEET PRINTING RESULTS
01
Sample
R 1
8 R 2
-H -P
*& c3
•« 1 R 3
O tn
4j Q. R 4
0)
* R 5
C 6
H C 7
0
]j C 8
c:
u C 9
CIO
(Gloss)
Ink
holdout
2
2
2

2

2
2
2

2
2
2
Strike-
through
3
2
2

2

2
2
2

2
2
2
Printing
(smoothness)
mottle
3
3
3

3

3
3
3

3
3
3
Ink
spread
(sharpness)
3
3
3

3

3
3
3

3
3
3
Show-
through
2
2
2

2

2
1
1

1
1
1
Total
12
12
12

12

12
11
11

11
11
11
         5.  Excellent    4.   Good   3.   Average   2.  Fair
1.   Poor

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                          SECTION XII

          POTENTIAL OF WET OXIDIZED, RECOVERED FILLER

                AS A POSSIBLE COATING PIGMENT


     When the recovered  filler obtained by wet 'oxidation was
dried, repulverized using a mortar and pestle, and pressed into
a pellet, it had an elrepho brightness of 81.4 percent.  This is
about equal to the brightness of filler grade clays but 5 to 6
points lower than conventional No. 2 coating clay.  Its lower
brightness would be its  first drawback as a coating pigment.

     The cooperating mill contracted with the Institute of Paper
Chemistry to have particle size distributions run on the recov-
ered filler.  These are  shown in Figure 5.  Its distribution lies
between that of a No. 2  coating clay and a filler clay.  Seventy-
four percent of the recovered clay is less than 2 um where a
No. 2 coating clay has 81 percent less than 2 ym.

     The recovered fillers dispersing agent requirement was
determined using a modification of TAPPI Procedure T648, using
sodium hexametaphosphate.  It did not readily disperse even when
treated with excessive quantities of the dispersant.

     Hercules viscometer rheograms taken on the wet oxidized,
recovered filler at 40 percent solids showed it required about
four times the shear stress to get the material to shear as com-
pared to No. 2 coating clay at the same solids level.

     The wet oxidized, recovered filler is a mixture of all of
the inorganic material which was in the deinking sludge before
wet oxidation.  Transmission electron photomicrographs done at
Western Michigan University illustrate this most readily.  The
recovered filler contained kaolin clay, calcium carbonate, titan-
ium dioxide and other unidentifiable material.

     It seems unlikely that this material would be suitable as
a coating pigment due to its heterogeneous nature, lower bright-
ness, particle size distribution and dispersion difficulties;
but it is suitable as a  filler clay substitute.
                               56

-------
       ioo-
in
-o
        80
        60
LJU
U
o;
ai
o_
         40
         20
                                                      NO, 2 COATING CLAY
                                 FILLER CLAY
                                                        WET OXIDIZED RECOVERED
                                                               FILLER
          Q| i i  i—i—i—i	L
                                          _L
J	L
                  50    30  20      10    6432     1.0 0.8

                           EQUIVALENT SPHERICAL DIAMETER/ MICRONS
                                                                       0.2
               0.1
            Figure  5.   Particle size distribution of wet oxidized recovered filler.

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                          SECTION XIII

                           REFERENCES
 1.  A Study of Practical Approaches to Utilization of Solids
     from Deinking Mill Waste.  NCASI Technical Bulletin No. 67.
     June 1954.

 2.  MacDonald, J.P., and J.W. Kenney.  Abrasiveness Test for
     Paper Fillers.  TAPPI, 32, No. 11.  November 1949.

 3.  Sludge Material Recovery System for Manufacturers of Pig-
     mented Papers.  Water Pollution Control Research Series.
     12040 FES  07/71.

 4.  Frank, R.D., and F.C. Schmutz.  A Proposed Test for Abra-
     siveness of Pigments and Paper Fillers.  TAPPI, 43, No. 7.
     July 1960.

 5.  The Relation Between Process Water Quality Characteristics
     and Its Reuse Potential in Combination Board Mills, Part
     III, Procedures for Determining Water Quality Characteris-
     tics in Paper and Board Manufacturing Water Reuse Programs.
     NCASI Technical Bulletin No. 282.  September 1975.

 6.  TAPPI Testing Procedures.  Technical Assosication of the
     Pulp and Paper Indsutry, Atlanta, Georgia.

 7.  Useful Methods.  Technical Association of the Pulp and Paper
     Industry, Atlanta, Georgia.

 8.  Personal Communications.  E. Grys, Technical Director,
     Fletcher Paper Company, Alpena, Michigan.

 9.  Personal Communications.  James E. Flynn, Manager Technical
     Services, Lock Haven, Pennsylvania.

10.  Personal Communications.  T. Collins, Research Chemist,
     Hammermill Paper Company, Erie, Pennsylvania.
                               58

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                          SECTION XIV

                          APPENDICES


                                                            Page

A.  Laboratory Evaluation of Recovery Techniques              60

B.  Details of Printing Trial and Evaluation for              74
    Coated Fine Paper Samples

C.  Details of Uncoated Web Offset Printing Trial and         76
    Printing Evaluation

D.  Details of Printing Evaluation of Uncoated Web            82
    Offset Samples from Wet Oxidized Recovered Filler
    Trial
                               59

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                           APPENDIX A

          LABORATORY EVALUATION OF RECOVERY TECHNIQUES


EXPERIMENTAL PROCEDURE

     The experimental design for this laboratory project was
divided into three main parts.  The first was to compare four
methods of recovering an acceptable filler grade clay from high
ash primary paper sludge.  These four methods were centrifugal
separation, foam flotation, screening and wet oxidation.  The
second part of the design was to evaluate the fillers recovered
from each method.  The percent filler, brightness and abrasive-
ness were determined in this evaluation.  The final part was to
make up handsheets for the two most promising techniques.  These
sheets were tested for their optical, strength and sizing pro-
perties .

     The high ash primary sludges used in this project were from
two different paper mills, both making printing and bond grades
of paper.  However, one mill was involved in deinking operations
and the other was not.  Enough  of both types of sludges were
stored in a refrigeration unit so that all of the recovery meth-
ods could be evaluated from the same sludge.

Recovery Methods

     All of the recovery method trials were done at Western
Michigan University and were run on both types of sludges.

Centricleaning—
     The centrifugal separation was done using a No. 600 3-inch
(7.62 cm) Bauer Centricleaner.  The inlet pressure and back
pressure were kept constant at 50 and 5 psig (340 to 34 kPa)
respectively.  The sludge was diluted to two consistencies, 0.1
percent and 0.5 percent.  Both the accepts and the rejects from
the cleaner were analyzed.

Foam Flotation—
     The foam flotation work was done in a Fegergran Lab Flota-
tion machine made by WEMCO (Western Machinery 'Company) .  The
surfactant, its concentration and the sludge conditioning had
been predetermined by work done by Prakasha Misra for his Senior
Thesis in conjunction with the NCASI.  The surfactant was a


                               60

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partially soluble, cationic quaternary ammonium chloride,
Kemamine Q-6502, which is produced by Humko Products.  Enough
sludge to yield 20 grams dry suspended solids was put into a
Waring Blender and broken up for 5 minutes.  Next the pH was
adjusted to 6.5 using dilute NaOH or H2S04.  The concentration
of the surfactant was 0.75 percent of the 20 grams suspended
solids.  The surfactant was added to the pH adjusted sludge and
then mixed well in the Waring Blender for 5 minutes at low speed.
Finally, the sludge was put in the flotation cell and diluted to
approximately 0.70 percent solids.  The air flow to the cell was
regulated to maintain a small bubble size and a supporting layer
of foam on the surface.  The flotation cell was run for 3 to 4
minutes and then the volume of both the froth and the tailings
were measured and analyzed.

Screening—
     The separation of the filler from the fiber by simple
screening was accomplished with 18-inch SWECO vibrating screen.
The sludges were diluted to 0.1, 0.4, 1.0, 2.0 and 3.0 percent
solids.  The sludge was placed over the vibrating screen at a
constant dry solids loading of .04 pounds per minute (18 gm/min).
Two screen mesh sizes, 230 and 325, were used at all five of the
percent solids levels.  The weight setting on the bottom of the
motor was kept at 20° so that the fiber would go out across the
screen rather than spiraling around the screen which tends to
trap the fillers.  Samples from the overflow and the flowthrough
were analyzed.

Wet Oxidation—
     The final method used to recover the fillers was wet oxida-
tion.  The sludge was diluted to 2 to 3 percent solids.  One
liter was poured into the stirred reactor built by Autoclave
Engineers and sealed.  Next, enough oxygen was added to bring
the pressure up to 500 psig (3400 kPa).  The conventional sludge
was brought up to 600°F (316°C)  and held there for 10 minutes.
The maxium pressure that developed during these cooks was 2900
psig (20,000 kPa).  The deinked sludge had to be heated up to
620°F (327°C)  for 30 minutes before complete oxidation took
place.  A maximum pressure of 3400 psig (23,000 kPa)  was re-
corded  during the deinked cooks.  After the bomb had cooled off,
it was vacuumed out and the contents analyzed.

Analysis of Recovered Fillers

     The recovered fillers were analyzed using the following
tests.

Percent Filler or Ash Content—
     The ash content was determined following TAPPI Standard
Method T-113.   A 15 percent loss of filler from ignition in the
muffle furnace was assumed in all of the calculations.
                               61

-------
Percent
     A modification  of TAPPI Standard Method T-439 m-60 was used
to find percent Ti02 of the recovered filler.  This modification,
which originated at  Du Pont, uses potassium pyrosulfate to fuse
the sample before  it is put into solution.

Brightness—
     A brightness  pad was  formed in a Buchner funnel, dried and
then measured  for  brightness using the elrepho brightness tester.
The brightness was reported percent elrepho.  For the wet oxida-
tion filler and the  standard water-washed clay filler, a special
disc was made  due  to the fact the dried fillers on the filter
paper cracked  badly.

Abrasion—
     The flat  disc method  proposed by Frank and Schmitz, modified
by the NCASI  (4,5) was used to find the relative abrasiveness
of solutions.  A felt wrapped around an abrading block which was
mounted in a drill press was placed in contact with a bronze
disc and rotated while the filler slurry was circulated over the
disc.  The relative  loss of weight of the disc measures the abra-
sion tendency  of the material.

Handsheet Procedures

     These samples of recovered fillers from the screening and
wet oxidation method were  used to make up laboratory handsheets.
These were compared  to sheets made with ones using a standard
water-washed Kaolin  filler clay.  The filled sheets contained
20 percent clay addition and no addition of Ti02 to give a target
filler content of  about 10 percent filler in the final handsheet.
All of the handsheets were made on the Noble and Wood handsheet
machine with target basis  weight of 60 gm/m^.  The furnish, 60
percent bleached softwood  kraft and 40 percent bleached hardwood
kraft, was refined in a Valley beater until Canadian Standard
Freeness of 350 was  reached.  The sheets were sized with 1.0
percent rosin and  2 percent alum.  The pH in the mixing tank and
in the sheet mold  kept close to 4.5 with dilute sulfuric acid.
They were conditioned overnight in a constant temperature and
humidity room, then  the following tests were run on them:

        TAPPI Standard Method               Test

                410                 Basis weight
                411                 Caliper
                452                 Brightness (elrepho)
                425                 Opacity
                494                 Tensile
                494                 % Stretch
                494                 Tensile energy absorption
                403                 Brust (Mullen)
                               62

-------
         TAPPI Standard Method                Test

                 414                Tear (internal)
                 511                Fold (MIT)
                 413                Ash Content
                                    Sizing - Hercules
                 499                IGT Pick
         TAPPI Useful Method        K and N Ink
                 553                Hiding power


     From the ash content of the handsheet, one pass filler re-
tention was calculated.  The tensile factor was calculated by
dividing the tensile by the basis weight.


DISCUSSION OF RESULTS

Centrifugal Separation

     Although centricleaners are quite widely used in the paper
industry as a method to separate solids from fibers, their appli-
cation as a filler recovery method did not prove to be fruitful.
From Tables 1-A and 2-A it can be seen that the maximum increase
in percent filler was only 8 to 10 percent.  Also, the inconsis-
tency in which the two sludges behaved seemed to bring out the
ineffectiveness of the centricleaners.  The conventional sludge
had a maximum purity in the first pass rejects at 0.5 percent
solids while the deinked sludge had its maximum purity in the
accepts after four passes through the cleaners at 0.1 percent
solids.  The fillers used in the handsheets were those recovered
in the first pass rejects at 0.5 percent solids for both sludges.

Foam Flotation

     From previous work done, it was found that 90  to 92 percent
of the filler materials could be recovered with purity increase
of 17 to 18 percent or a total purity of 75 to 80 percent.  The
work done on flotation for this project was also aimed at these
figures but with a different flotation cell.  The Fergergran
laboratory flotation cell was a larger unit and it  did not have
the exact control over the bubble size that the previously used
cell had.  However, we did match results very closely as the
figures of Tables 3-A  and 4-A point out.  The conventional
sludge had a purity of 75 percent and a  recovery of 90 percent.
The deinked sludge was somewhat lower with a purity of 61.5 and
a recovery of 70.5.  The main variable with the Fergergran cell
was the length of time that each batch should be run, because
the purity decreased with time.  By taking samples  at 1-minute
intervals, the purity  and recovery was found throughout the
transition of a flotation run.  Figure 1-A is a plot of purity
                                63

-------
Table 1-A.   RECOVERED FILLER PURITIES FROM
  CENTRIFUGAL  SEPARATION DEINKING SLUDGE
Centricleaner Pass
Raw sludge
At 0.5% solids
1st pass: accepts
1st pass: rejects
2nd pass: accepts
2nd pass: rejects
3rd pass: accepts
3rd pass: rejects
4th pass: accepts
4th pass: rejects
At 0.1% solids
1st pass: accepts
1st pass: rejects
2nd pass: accepts
2nd pass: rejects
3rd pass: accepts
3rd pass: rejects
4th pass: accepts
4th pass: rejects
Total
solids %
28.5

0.38
1.59
0.38
0.88
0.36
0.69
0.35
0.58

0.11
0.52
0.11
0.20
0.10
0.15
0.10
0.13
Ash,
%
45.0

53.5
34.4
51.8
33.9
53.8
39.3
54.2
41.5

52.7
27.0
55.9
38.1
57.0
43.7
57.9
50.1
Filler,
%
52.9

62.9
40.5
61.0
39.9
63.3
46.2
63.7
48.8

62.0
31.8
65.7
44.9
67.1
51.4
68.1
59.0
Fiber,
%
47.1

37.1
59.5
39.0
60.1
36.7
53.8
36.3
51.2

38.0
68.2
34.3
55.1
32.9
48.6
31.9
41.0
                      64

-------
Table 2-A.  RECOVERED FILLER PURITIES  FROM
CENTRIFUGAL SEPARATION  CONVENTIONAL SLUDGE
Centricleaner pass
Raw sludge
At 0.5% solids
1st pass: accepts
1st pass: rejects
2nd pass: accepts
2nd pass: rejects
3rd pass: accepts
3rd pass: rejects
4th pass: accepts
4th pass: rejects
At 0.1% solids
1st pass : accepts
1st pass: rejects
2nd pass: accepts
2nd pass: rejects
3rd pass: accepts
3rd pass: rejects
4th pass: accepts
4th pass: rejects
Total
solids %
4.91

0.40
2.52
0.40
0.94
0.39
0.64
0.40
0.57

0.11
0.72
0.11
0.20
0.10
0.16
0.09
0.13
Ash,
%
55.0

49.4
61.8
49.3
46.2
49.5
45.4
49.0
48.6

51.9
53.3
52.9
44.0
54.1
45.4
53.5
48.8
Filler,
%
64.7

58.2
72.7
58.0
54.3
58.3
53.4
57.6
57.2

61.1
62.7
62.3
51.8
63.7
53.5
62.9
56.4
Fiber,
%
35.3

41.8
27.3
42.0
45.7
41.7
46.6
42.4
42.8

38.9
37.3
37-7
48.2
36.3
46.5
37.1
42.6
                     65

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     Table 3-A.  SUMMARY OF HIGH ASH SLUDGE
  LABORATORY RECOVERY TECHNIQUE DATA - PURITY
    (% of product which is filler material)
Separation
technique
Original sludge
Centricleaning
Screening
Foam flotation
Wet oxidation
Conventional
s ludge
%
48.0
72.7
91.5
75.5
100.0
De inking
sludge
%
52.9
62.9
76.5
61.5
100.0
     Table 4-A.  SUMMARY OF HIGH ASH SLUDGE
  LABORATORY RECOVERY TECHNIQUE DATA - RECOVERY
(% of filler in original sludge which is recovered)
Separation
technique
Centricleaning
Screening
Foam flotation
Wet oxidation
Conventional
sludge
%
1.5
97.7
90.5
100.0
Deinking
s ludge
%
98.3
97.3
70.5
100.0
                       66

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90--
                             % RECOVERY  OF  FILLER

                             % PURITY OF  FILLER
• i®-
       ~®—
                           TIME  IN  MINUTES


         Figure 1-A.  Foam flotation:  time  vs.  %  filler
                      purity  and recovery

-------
and recovery versus time.  From this figure, it was decided that
a batch run would be 3 to 4 minutes long.

Screening

     Figure 2-A summarizes all of the work done with the SWECO
vibrator screen.  It shows how the recovery for both sludges was
very high with 96 percent minimum and that the 325-mesh and 230-
mesh lines were almost the same.  This means the 230-mesh screen
was just as effective as the 325-mesh screen for the recovery of
the filler.  An analysis of variance was run to find out if the
percent solids, mesh size or their interaction significantly
affected the purity and the recovery.

     At a 95 percent confidence level, neither the mesh size nor
their interaction affected the purity or the recovery.  However,
as the percent solids increased, the purity also increased.
Although recovery decreased slightly with increasing solids, it
was not significant at a 95 percent confidence level.

Wet Oxidation

     The conditions for wet oxidation were chosen to ensure a
complete oxidation of all fibrous materials.  At these extreme
conditions, the purity and recovery were both 100 percent.

Summary of Separation Results

     A final summary of the methods of recovering filler materi-
als  from high ash primary sludge is shown in Tables 3-A and
4-A.  Wet oxidation and screening have high recovery for both
types of sludges.  The purity of the deinked sludge was lower
than the conventional sludge in every method except wet oxida-
tion.  The centricleaners and vibrating screen were much easier
unit operations to run.  Because of its high recovery with either
sludge, good purity and ease of operation, screening appeared to
be the best method to recover the filler material from the
sludge.

     In Table 5-A the brightnesses of the recovered filler for
both sludges is listed.  When these were compared to a standard
filler clay which has a brightness of 81 to 82 percent elrepho,
it was decided that the recovered filler would probably cause
some loss in sheet brightness when employed.

Abrasiveness

     One of the main concerns in reusing the filler was that the
filler would become more abrasive.  From Table 6-A it can be
seen that the fillers from wet oxidation were more abrasive than
the filler from the other methods.  However, the relative


                               68

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10
                                           % FILLER RECOVERY
           FOR BOTH
                                     FILLER PURITY OF
                                                       CONVENTIONAL SLUDGE
    DEINKED - MESH
    DEINKED - MESH 230
CONVENTIONAL MESH  325	O
CONVENTIONAL MESH  230	«
                                    % FILLER PURITY OF DEINKED SLUDGE
                               	-—- __»— —
            ®
                                       CONSISTENCY OF SLUDGE

                     Figure 2-A.   Screening.   The effect of screen mesh and
                              consistency on purity and recovery.

-------
         Table  5-A.   BRIGHTNESS RESULTS
                    (Elrepho)
Separation tech .
Raw sludge
Centricleaners
Screening
Flotation
Wet oxidation
De inking
50.8
54.5
56.0
50.6
73.5
Conventional
63.0
61.1
71.3
71.7
71.7
Table 6-A.  ABRASION RESULTS BY FLAT DISC  METHOD
Sample
Filler grade clay
Filler grade clay
Centricleaned sludge
Screened sludge
Foam floated sludge
Wet oxidized sludge
Slurry
consistency
%
10
6
6
10
6
10
De inking
wt loss
(mg/disc)
7.1
6.3
1.4
4.1
1.3
6.4
Conventional
wt loss
(mg/disc)
7.1
6.3
1.0
4.2
2.4
7.0
                        70

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abrasiveness of the filler from any of the methods was not
greater than a normal filler grade clay.

Effect of Screened and Wet Oxidized Recovered Filler on
Physical and Optical Properties of Hand Sheets

     Contained in Tables 7-A and 8-A are the results of handsheet
tests made employing filler recovered by the screening and wet
oxidation techniques for the conventional and the deinking mill
sludges.  The blocked figures are numbers which were shown to be
statistically lower than the control at a 99.5 percent confidence
level using the t test.  The only property of practical concern
which changed was the brightness.  The screened, recovered filler
caused a drop of 3.6 points for the conventional sample and 10.9
points for the deinking sample.  The 3.6 drop in brightness may
be able to be tolerated but certainly not the 10.9 drop.  Thus,
it appears that from a laboratory handsheet viewpoint, screening
for filler recovery may be a possibility for a mill not practic-
ing deinking.  Wet oxidation will be the route a deinking mill
will probably have to pursue.  None of the other physical or
optical properties tested seem to be affected.
                               71

-------
 Table 7-A.  HAND SHEET PROPERTIES MODIFICATION
                  (conventional)
Property
Basis wt. (G/M2)
Caliper (.0*01 in.) /(mm)
Brightness (elrepho)
Opacity (TAPPI)
Tensile (Kg)
Tensile factor (Kg M2/gm)
Stretch (%)
Tear (gm)
Mullen (PSI)/(kPa)
Fold (number)
Hercules size (sec)
Filler (%)
Retention (%)
IGT Pick
Hiding power
K & N Ink (% red.)
Control
64.6
5.41/0.137
72.5
83.6
7.98
0.125
2.64
52.8
22.6/156
21
66.5
9.4
46.9
255
0.77
46.3
Screened
64.4
5.38/0.137
|68.9| a
87.6
7.99
0.126
2.62
48.0
24.3/167
30
35.9
10.9
54.6
245
0.87
50.8
Wet-oxidized
[6374] a
5.22/0.133
73.4
85.4
7.59
0.119
2.54
56.8
25.8/178
34
118.5
11.4
56.9
245
0.85
53.3
Significantly different from control at  99,
confidence.
                       72

-------
 Table 8-A.  HAND SHEET PROPERTIES MODIFICATION
                   (deinking)
Property
Basis wt. (G/M2)
Caliper (.001 in.) /(nun)
Brightness (elrepho)
Opacity (TAPPI)
Tensile (Kg)
Tensile factor (Kg M/gm)
Stretch (%)
Tear (gm)
Mullen (PSI)/(kPa)
Fold (number)
Hercules size (sec)
Filler (%)
Retention (%)
IGT Pick
Hiding power
K & N Ink (% red.)
Control
64.6
5.41/0.137
72.5
83.6
7.98
0.125
2.64
52.8
22.6/156
21
66.5
9.4
46.9
255
0.79
46.3
Screened
[63T7]a
5.39/0.137
|61. 6|a
92.1
7.52
0.117
2.42
48.8
23.7/163
27
72.7
12.1
60.6
255
0.93
47.5
Wet-oxidized
HsTTsl a
5.28/0.134
75.2
89.1
7.50
0.122
2.16
55.2
20.0/138
13
77.1
10.9
5.4
230
0.88
54.8
Significantly different from control at 99
confidence.
                      73

-------
                           APPENDIX B

            DETAILS OF PRINTING TRIAL AND EVALUATION

                  FOR COATED FINE PAPER SAMPLES


ASSESSMENT OF PRINTING QUALITY OF COATED OFFSET PRINTED
SAMPLES CONDUCTED BY E.W. RAYFORD

     The absence of standards upon which the characteristics of
printability of the test sheets could be based, limits the com-
prehensiveness of this evaluation.  In this case, the separate
test sheets were evaluated one against the other in an attempt to
arrive at comparative values.

     The primary difficulty encountered in the evaluation was
the poor quality of the printing.  Sharpness and gloss were two
of the characteristics to be evaluated.  Close examination with
10X, 12X and 30X glasses revealed more than minimal differences
in these two characteristcis between the samples.  Color, gloss
and sharpness are a function of the amount of ink laid on the
sheet.  Inspection revealed visible differences in ink coverage
and color.  Not knowing the printing sequence of the samples, I
was unable to determine whether the differences were due to pa-
per factors or press problems.  After determining that there was
little difference in the amount of showthrough and strikethrough
between the samples, and that the printing quality was markedly
different on the back sides of some of the samples, I decided to
run a series of densitometer readings on the four process colors.
These curves showed wide latitudes in color control on the press.
Correlations can be drawn between the amount of ink on the sheet
and the differences in penetration and gloss, and printing
sharpness.

     Examination of the slur gauges also reveals press problems.
Good dot hardness and sharpness is most often a result of good
press conditions.  Evidence of the word "slur" o^all of the
samples indicates less than optimum printing quality.  Examina-
tion of both highlight and shadow dots under a 30X glass indi-
cates soft, mushy and slurred dot formation, particularly on the
blue and black.  This would result in.a lack of printing sharp-
ness and halftone quality.
                               74

-------
     A certain amount of scumming is apparent on many of the
samples.  I think this can also be attributed to press conditions
rather than to paper factors.

     The mis-register also lowers the quality of the printed job
and the determination of fine detail.

     After making close examinations of both sides of each sam-
ple, and close comparisons between the samples, keeping in mind
the lack of uniformity of press control, I found no major differ-
ences in the printability of the samples.  Samples 14, 17 and 26
were less opaque; and samples 21, 23 and 26 in particular, lacked
sharpness in the halftones.  There were little apparent differ-
ences in strikethrough, mottle, pick resistance, fiber puffing
and blister, and ink spread.  These were all considered to be
satisfactory.  Opacity was considered to be somewhat low in all
samples where there was no backup, particularly samples 23
through 26, bvit showthrough was not evident when backed up with
light colors.

     One characteristic noticed was the softness of the samples
and the lack of resistance to tear in handling.

     In my opinion, the printing characteristics of all of these
samples were satisfactory, and that most of the objectionable
qualities found in the printing were due to press conditions.
However, whether or not these conditions could be controlled to
a closer degree on the press using these papers cannot be ascer-
tained  from these samples, but should be determined from the
reports of the press conditions and paper runability.
                                75

-------
                           APPENDIX C

         DETAILS OF UNCOATED WEB OFFSET PRINTING TRIAL

                    AND PRINTING EVALUATION


ASSESSMENT OF PRINTING QUALITY OF UNCOATED FINE PAPER PRINTED
SAMPLES CONDUCTED BY E.W. RAYFORD

     An honest and genuine attempt was made to evaluate the
printing qualities of the thirty-five samples submitted to me.
Because of wide variation in the quality of the printing and ink
coverage, I  feel the evaluation of the printing quality of the
paper is subject to some question.

     The differences, in my opinion, were due more to printing
quality and  press condiitons than to paper characteristics.  Of
course, there is a big difference between most of the printing
qualities of the lightweight stocks and the heavier weight
stocks.

     Because of the imposition of the backup forms, evaluation
of some qualities were limited.  The solid color bars were backed
up by another bar of the same color; the black halftones were
backed up by the GRETAG Control Bar; large color areas, screens
and process  were backed up by large color areas.  Therefore,
strikethrough and showthrough were confined to limited areas.
The amount of strikethrough, showthrough and lack of ink holdout
was in most  cases, directly related to the amount of ink
applied.  Color density could be expected to be greater in the
color bars because of being backed up by the same color, parti-
cularly in the lighter weight stocks.

     Printing sharpness was evaluated in the half tones and the
screened areas.  Because of the large differences in ink cover-?.
age, evidence of plate wear and breakdown, and other printing
factors, I think sharpness was more a condition of printing
quality than paper quality.  An additional twenty-two samples
were added to the original thirty-five to give me a better exam-
ple of plate image breakdown, but because these samples too,
were randomized, they had no more meaning than the original
thirty-five.  Where ink coverage was light and the plate new,
sharpness was good in all categories, highlights, mid-tones and
shadows.  As the run progressed, all areas got progressively


                               76

-------
worse, particularly when ink coverage was heavier.  It was also
noted to deteriorate more in the shadow areas where dot structure
disappeared entirely in some areas.

     A special effort was made to evaluate the printing sharpness
in the halftones on the additional samples which were used to
assess the importance of plate wear on printing.  Highlights,
midtones and shadows were evaluated, and recorded individually
as well as the average overall sharpnes.  It should be noted
that there was little, if any difference noted between these
samples and the other thirty-five samples.  The same faults, too
little or too heavy ink coverage, dot breakdown and loss of
shadow dot detail, slur and scum are all evident in various sam-
ples .   Densitometer readings were recorded for the black on these
samples in an attempt to relate the amount of ink coverage with
printing sharpness.  No densitometer readings were recorded for
the other three colors on these samples.

     As a whole, I would say printing sharpness was poor, except
in a few cases.  However, these conditions were noted to be sim-
ilar on all paper samples, with the difference between weights
again being noted.

     Printing smoothness or mottle was evident in the blue on all
samples, and in the black on some samples where the ink coverage
was heavy.  The other colors were good.

     Ink spread was noted on the head of the red color bar in
some cases, and on the tail of this same color bar on others. It
was noted on the tail of the black bar on several samples.  Also,
the dot structure of the screens was noted to be soft on many
samples.  This could be a condition of ink spread or dot slur.
The SLUR gauges were noted as being bad on many samples.

     Ink coverage was very inconsistent, both between samples,
and in many cases, within a sample.  In some cases, coverage
was very light, the paper showed through the ink so badly that
no evidence of solid coverage was apparent.  On these samples,
sharpness was rated accordingly higher.  Ink coverage can be
noted on the densitometer charts.

     There was a good deal of black ink transfer on the other
colors caused by press rollers.  There was also scumming evident.
This made taking densitometer readings in some areas impractical.

     Register is bad on many of the process samples, and is also
evident in the back-up of the Control Strip.

     In my opinion, the average quality of the printing is low,
but I think this is due to press conditions and problems as
similar faults are evident on all of the different types of
paper, the  exception being between the lightweight papers and

                               77

-------
the heavier papers.  Quality, overall, is lower on the lighter
weight samples.

     There was little, if any, evidence of fiber pick on any of
the samples.

     In all cases, the lightweight and the heavier weight samples
were separated for evaluation, but samples within the separate
weights were randomized.  The charts are sequential for ease of
recording.  (See Table 11 in "Discussion of Results" Section.)

Densitometer Readings
Macbeth RD-100

     Densitometer readings were taken in several areas: on the
solid patch of the Control Strip, in the center of the solid
color square, and on the left end, center and right end of the
solid color bar.  As the yellow GRETAG color patch, the color
square and the left end of the solid color bar are all in line
of press travel, these densitometer readings were the same.
However, by moving the aperture about one and one-half inches to
the right, a much higher reading was obtained.  This difference
is noted between the columns marked GRETAG and Color Bar, left
on the yellow.

     Also, differences in color values could be obtained on all
colors by moving the aperture fractions of an inch.  Therefore,
a special effort was made to read the same respective area on all
colors on all samples  (except as noted above on the yellow).

     Areas marked NG could not be recorded, either because the
area was contaminated with another color, mostly black, or
showthrough of mis-register on the lighter samples made the
reading meaningless.
                                78

-------
DENSITOMETER READINGS








Sample
number
1.
2.
3.
4.
5.
6.
7.
8.
9.
.10.
11.
12.
13.
14.
15.
16.
17.
18.
19.
20.
21.
22.
23.
24.
25.
26.
27.
28.
29.
30.
31.
32.
Yellow




0)
n n a
So u
•H 41
tr o id
w o o
0.82
0.82
0.82
0.80
0.82
0.87
0.90
0.88
0.86
0.87
0.86
0.90
0.90
0.92
0.90
0.87
NG
0.88
0.86
NG
0.92
0.93
0.92
0.94
0.94
0.92
0.92
0.88
0.87
0.85
0.92
0.90

Color bar




4>

Si

2
0.84
0.88
0.86
0.87
0.86
0.92
0.93
0.94
0.92
0.90
0.88
0.92
0.90
0.94
0.90
0.86
0.90
0.98
0.90
0.89
0.94
0.95
0.94
0.94
0.98
0.95
0.98
0.96
0.94
NG
NG
Magenta




0)
M M X
id o u
P i— 1 4J
O1 o id
w o a
0.93
0.94
0.99
1.04
1.04
1.14
1.12
1.10
0.98
1.04
0.95
1.01
1.02
1.00
0.98
1.12
1.11
1.15
1.10
1.04
0.99
1.00
1.02
0.98
1.00
1.08
1.06
1.06
1.10
1.07
1.04

Color bar




4>

tr o id
M u a
1.20
1.21
1.22
1.18
1.15
1.19
1.18
1.24
1.16
1.14
1.06
1.14
1.01
1.14
1.16
1.22
1.20
1.16
1.18
1.20
1.20
1.28
1.26
1.21
1.25
1.16
1.23
1.24
1.30
1.25
1.02 1.25
1.04 1.24

Color bar




4J
 O id
M o a
1.U4
1.02

Color bar




4>

,£2
tr>
•H
K
l.Ub
1.11
1.07
1.10
1.02
1.18
1.22
1.20
1.10
1.14
1. 30
1.35
1.38
1.38
1.34
1.34
1.30
1.32
1.34
1.38
1.21
1.20
1.28
1.29
1.26
1.46
1.38
1.44
1.42
1.34
1.39
1.41
GRETAG - HIT
Color control
system




rH
iH
d)
U.U2
0.82
0.82
0.80
0.82
0.87
0.90
0.88
0.86
0.86
0.86
0.88
0.90
0.92
0.90
0.87
0. 88
0.88
0.86
0.88
0.92
0.93
0.92
0.94
0.94
NG
NG
NG
NG
NG
NG
0.90

id
4J
C
O
O1
id
u.uy
0.88
0.90
0.92
0.97
1.08
1.06
1.07
0.92
0.98
0.86
0.94
0.94
0.96
0.94
1.06
1.06
1.04
1.10
1.06
0.96
0.94
NG
0.96
0.99
0.98
1.01
NG
NG
NG
0.96
1.00






"
l.l/
1.11
1.13
1.14
1.15
1.15
1.10
1.14
1.11
1.06
1.02
1.10
1.12
1.04
1.04
1.16
1.06
1.11
1.16
1.14
1.12
1.14
1.18
1.12
1.14
1.07
1.22
1.18
1.20
1.17
1.18
1.14



^
o
id
1-1
1.00
1.02
1.00
1.00
1.04
1.32
1.26
1.33
1.20
1.22
1.25
1.28
1.28
1.28
1.26
1.34
1.35
1.32
1.32
1.36
1.20
1.20
1.40
1.32
1.28
1.39
1.42
1.41
1.36
1.32
1.40
1.50

-------
DENSITOMETER READINGS
     (continued)




Sample
number
33.
34.
35.
Highes
Lowest
Range
Yellow


o>
v< M .c
n) O (J
3 rH 4J
O1 o m
U) U 0
0.90
0.93
0.94
0.94
0.80

Color bar

4J
M-l
a
1.04
1.06
1.04
1.08
0.91
i<
Cente
1.08
NG
NG
1.10
0.98

&
tj>
•rH
«
0.96
0.99
0.98
0.99
0.84
0.. 80-1. 10
Magenta


0)
fc M £
ra o o
3 H 4J
tr o it
en u a
1.00
1.02
1.05
1.15
0.93


Color bar

.u
H-l
3
0.95
1.01
0.96
1.14
0.86
M
Cente
.
1.08
1.20
1.18
1.24
0.99

-P
D>
2
1.06
1.10
1.14
1.17
0.86
0.86-1.24
Cyan


H
3
1.18
1.05
1.00
1.18
0.91
u
Cente
1.24
1.14
1.12
1.36
1.02
0.91-1.30

jj
•&
•H
K
1.21
1.10
1.12
1.22
0.98

Black


01
^ M j:
n) O u
3 rH 4J
tj< 0 <8
u> u o,
1.4S
1.47
1.46
1.48
1.00

Color bar

4-1
IM
3
1.33
1.24
' 1.40
1.34
0.91
n
Cente
1.44
1.55
1.54
1.56
1.14

4J
•a
a
1.40
1.50
1.41
1.50
1.06
0.91-1.56
GRETAG - RIT
Color control
system
2
Yello
NG
NG
NG
0.94
0.80
0.14
id
4J
01
I
0.98
NG
1.00
1.10
0.86
0.24

n)
&
1.24
1.06
1.04
1.24
1.07
0.17

Black
1.47
1.34
1.46
1.50
1.00
0.50

-------
                                      DENSITOMETER READINGS
oo
Sequen-
tial
Samples


Sample
number

Al
A2
Bl
B2
Cl
C2
Dl
D2
El
E2
Fl
F2
Gl

G2
HI
H2
11
12
Jl
J2
Kl
K2
Highest
Lowest
Range
Yellow














Q
w
§
o
o
s

EH
o
2










Magenta














Q
W
§
o
U
s


o
2










Cyan














Q
W
o
U
3

EH
o
2










Black


(!)

nJ O O
3 H -P
tT< O (U
C/) O fit
Ma
1.35
1.31
1.26
1.24
1.40
1.24
1.40
1.42
1.52
1.44
1.48
1.44

1.50
1.40
1.44
1.43
1.48
NG
1.45
1.40
1.43
1.52
1.24


Color bar


-P
m
0)

0.86
1.20
1.26
M
1.17
1.32
1.22
1.26
1.34
1.46
1.44
1.34
1.28

1.34
1.36
1.24
1.30
1.34
1.16
1.22
1.20
1.16
1.46
0.86
H
0)
-P
d)
u
1.14
1.27
1.32
M
1.16
1.34
1.36
1.40
1.34
1.54
1.54
1.54
1.50

1.60
1.46
1.53
1.60
1.56
1.32
1.46
1.51
1.48
1.60
1.14

p

-H
«
0.94
1.23
1.30
1.18
1.19
1.32
1.21
1.41
1.41
1.38
1.40
1.52
1.34

1.46
1.38
1.42
1.56
1.47
1.22
1.28
1.39
1.38
1.56
0.94
0.86-1.60
GRETAG - RIT
Color control
system
>
O
H

*







Q
W
§
o
U
$

EH
o
2












i m
tri-p

S 
-------
                           APPENDIX D

           DETAILS OF PRINTING EVALUATION OF UNCOATED

  WEB OFFSET SAMPLES FROM WET OXIDIZED RECOVERED FILLER TRIAL
                                  I

ASSESSMENT OF PRINTING QUALITY OF UNCOATED WEB OFFSET
PRINTED SAMPLES CONDUCTED BY E.W. RAYFORD

     A lack of standards limits the evaluation of these test
sheets.  The uncoated samples also appeared to have very similar
properties of printability.  All of the colors except black are
screened, and most of them are arrived at through a combination
of two or more screened colors; therefore, mottle, spread, and
printing sharpness were more easily determined using the black
printed areas.

     Printing sharpness is satisfactory on all of the samples.
Again, there is evidence of soft, mushy screen patterns but this
was found to be similar on all of the samples.  There was little
evidence of ink spread into the unprinted areas.

     Gloss was considered to be low on all colors except the
black where it was judged to be satisfactory.  There is evidence
of scumming throughout the samples, more so on the black than
on the other colors.  This was attributed to press conditions
such as ink-water balance (this could also be a factor in the
low gloss) , counter etching of the plate, or other plate or
press factors.  The higher gloss of the black and the larger
amount of scumming could be a result of a heavier ink flow.

     Printing smoothness was considered to be average for a
base sheet such as this.

     Opacity was considered to be poor.  The amount of show-
throught is objectionable, even when backed up.  Samples 6
through 10, the control samples, were considered to be slightly
worse than samples 1 through 5, the recovered filler samples.

     There is evidence of strikethrough on all of the samples.
The amount of strikethrough and the lack of opacity and gloss
would, in my opinion, determine ink holdout to be only fair.

     The printability of these sheets was considered to be sat-
isfactory except in the areas of strikethrough and showthrough.

                               82

-------
Table 1-D.  PRINTING  SAMPLE EVALUATION
     BY USE OF  1-5  GRADING SYSTEM

Sample
1
2
3
4

5
6
7
8
9
10

(Gloss)
Ink
Holdout
2
2
2
2

2
2
2
2
2
2

Strike
Through
2
2
2
2

2
2
2
2
2
2

Printing
(Smoothness)
(Mottle)
3
3
3
3

3
3
3
3
3
3

Ink
Spread
(Sharpness)
3
3
3
3
*
3
3
3
3
3
3

Show
Through
2
2
2
2

2
1
1
1
1
1
                   83

-------
 1. RtPOHT NO.

 _  EPA-600/2-77-123
                              TECHNICAL REPORT DATA
                        (Please read Instructions on the reverse before completing:)
2.
                         3. RECIPIENT'S ACCESSION-NO.
 -: TITLE AND SUBTITLE

 INVESTIGATION OF REUSE POTENTIAL OF ASH FROM
 PAPERMILL SLUDGES
                         5. REPORT DATE
                          July 1977 issuing date
                         6. PERFORMING ORGANIZATION CODE
 7. AUTHOR13)
 Allan  M.  Springer, Duane  W.  Marshall, Isaiah
 Cellman
                                                  8. PERFORMING ORGANIZATION REPORT NO.
9. PERFORMING ORGANIZATION NAME AND ADDRESS
 National Council of the  Paper Industry for Air
     and Stream Improvement,  Inc.
 Central-Lake States Regional Center
 Kalamazoo, Michigan    49008
                         10. PROGRAM ELEMENT NO.
                          1BB610
                         11. CONTRACT/GRANT NO.


                         EPA-R-803348-01
 12. SPONSORING AGENCY NAME AND ADDRESS
 Industrial Environmental Research Lab.-Cin., OH
 Office of Research and Development
 U.S. Environmental Protection Agency
 Cincinnati, Ohio   45268
                         13. TYPE OF REPORT AND PERIOD COVERED
                         14. SPONSORING AGENCY CODE
                            EPA/600/12
 15. SUPPLEMENTARY NOTES
 16. ABSTRACT
       Two techniques  for recovery of filler  from fine papermill high ash
  sludges, screening and wet oxidation, were  evaluated for their technical!
  feasibility.  The alternative of screening  the  sludge and using the     I
  material passing through the screen as recovered filler was investigated
  in  cooperation with  two mills.  The screening  for recovery of filler
  was conducted at the mill site.  Then the material was shipped to
  Western Michigan University where selected  grades incorporating the
  recovered filler were manufactured.    The  paper manufactured was
  shipped to Rochester Institute of Technology where it was printed on
  their web offset press.  The grades simulated were found lacking only ir
  that the brightness  of the paper was from four  to seven points lower
  than grades made with virgin  filler.  The wet  oxidation alternative
  was evaluated in a  similar manner with a cooperating mill.  The wet
  oxidized recovered  fillers only slightly lowered the brightness of the
  sheet simulated and gave an increase in opacity in exchange.  The wet
  oxidation scheme appears technically feasible.   The screening alterna-
  tive would  probably have to  incorporate a  bleaching step before it
  would be deemed acceptable.   The technical  feasibility of oxidative
  bleaching was demonstrated.        	
17.
                           KEY WORDS AND DOCUMENT ANALYSIS
               DESCRIPTORS
                                       b.lDENTIFIERS/OPEN ENDED TERMS
                                    c. COSATI Field/Group
 Sludge,  clay minerals,  refractories,
 kaolin,  opacifiers,  fillers, paper-
 making,  paper mills, book paper,
 oxidation, screening,  separation,
 vibrating screens, recovery,
 reclamation
               Fine paper,
               Wet oxidation
 13/B,H
 11/B
 07/A
13. DISTRIBUTION STATEMENT

  Release To Public
              19. SECURITY CLASS (This Report)
               Unclassified
94
              20. SECURITY CLASS (Thispage)
               Unclassified
                                    22. PRICE
EPA Form 2220-1 (9-73)
                                     84
                                * ui GWBtfaexr ™Dmne omcE an- 757-ffl56/646»

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