Tennessee
Valley
Authority
United States
Environmental Protection
Agency
Office of Power
Power Research Staff
Chattanooga. Tennessee 37401
Office of Research and Development
Office of Energy. Minerals, and Industry
IERL. Research Triangle Park. NC 27711
EPA-600/7-76-021
                                          October 1976
TVA'S 1-MW PILOT PLANT
VERTICAL DUCT MIST
ELIMINATION TESTING
Progress Report
Interagency
Energy-Environment
Research and Development
Program Report

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                       RESEARCH REPORTING SERIES
Research reports of the Office of Research and Development, U.S.
Environmental Protection Agency, have been grouped into seven series.
These seven broad categories were established to facilitate further
development and application of environmental technology.  Elimination
of traditional grouping was consciously planned to foster technology
transfer and a maximum interface in related fields.  The seven series
are:

     1.  Environmental Health Effects Research
     2.  Environmental Protection Technology
     3.  Ecological Research
     4.  Environmental Monitoring
     5.  Socioeconomic Environmental Studies
     6.  Scientific and Technical Assessment Reports (STAR)
     7-  Interagency Energy-Environment Research and Development

This report has been assigned to the INTERAGENCY ENERGY-ENVIRONMENT
RESEARCH AND DEVELOPMENT series.  Reports in this series result from
the effort funded under the 17-agency Federal Energy/Environment
Research and Development Program.  These studies relate to EPA's
mission to protect the public health and welfare from adverse effects
of pollutants associated with energy systems.  The goal of the Program
is to assure the rapid development of domestic energy supplies in an
environmentally—compatible manner by providing the necessary
environmental data and control technology.  Investigations include
analyses of the transport of energy-related pollutants and their health
and ecological effects; assessments of, and development of, control
technologies for energy systems; and integrated assessments of a wide
range of energy-related environmental issues.
This document is available to the public through the National Technical
Information Service, Springfield, Virginia  22161.

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                                           PRS - 14
                                           EPA-600/7-76-021
                                           October  1976
           TVA'S  I-MW   PILOT  PLANT«

       VERTICAL DUCT  MIST  ELIMINATION

          TESTING  --  PROGRESS REPORT
                            by

G.A.  Hollinden,  R. F.  Robards,  and   N.D. Moore  (TVA/Chattanooga)
        T. M. Kelso  and  R. M. Cole  (TVA/Muscle Shoals)
                Tennessee  Valley Authority

                  Power  Research Staff
               Chattanooga, Tennessee  37401

                            and

         Office  of Agricultural and   Chemical  Development
                 Muscle Shoals,  Alabama  35660
        Interagency  Agreement  No.  EPA-IAG-D5-072I
               Program  Element No.  EHB528


            EPA  Project  Officer:  John  E.  Williams

          Industrial  Environmental Research Laboratory
           Office  of  Energy, Minerals,  and  Industry
              Research  Triangle  Park, NC  27711


                        Prepared  for:

          U.S.  ENVIRONMENTAL PROTECTION AGENCY
             Office  of   Research  and  Development
                    Washington, DC   20460

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                              DISCLAIMER






This report has been prepared by the Tennessee Valley Authority and




reviewed by the U.S. Environmental Protection Agency and approved for




publication.  Approval does not signify that the contents necessarily




reflect the views and policies of either agency, nor does mention of




trade names or commercial products constitute endorsement or




recommendation for use.
                                  ii

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                            ABSTRACT

TVA has recently demonstrated washing techniques that maintain con-
tinuous mist eliminator performance for lime/limestone closed-loop
scrubbing systems at its 1-MW pilot plant at the Colbert power
plant.  The systematic test program which developed these washing
techniques is reviewed for both the limestone and lime systems.
Continuous operation of the Chevron-type mist eliminator, positioned
horizontally in a vertical duct, in the limestone system was main-
tained (after extensive testing) by washing the bottom of the mist
eliminator intermittently with all the available clarified liquor
immediately followed by an allocated amount of the allowable makeup
water.  The top of the mist eliminator was washed intermittently
with the remaining allocation of allowable makeup water.  Contin-
uous mist eliminator performance in the lime system was maintained
by washing the bottom of the mist eliminator intermittently with
an allocated amount of allowable makeup water.  The remainder of
the allocated makeup water was used to intermittently wash the top
of the mist eliminator.
                                iii

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                            CONTENTS

                                                          Page
Abstract	iii
Figures  	   v
Introduction	   1
Summary and Conclusions	   2
Work Completed	   ^
Future Work	22
Conversion Factors 	  23
                                 iv

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                             FIGUKES

Humber                                                      Page
  1    TCA Scrubber Flow Diagram	k
  2    Chevron Mist Eliminator	5
  3    Mist Eliminator Test Module	6
  h    Top and Bottom Views of Mist Eliminator After 202
       Hours of Operation (Test ME-10)	8
  5    Top and Bottom Views of Mist Eliminator After 120
       Hours of Operation (Test ME-ll)	9
  6    Side and Bottom Views of Mist Eliminator After 96
       Hours of Operation (Test ME-12)	10
  7    Side and Bottom Views of Mist Eliminator After 8k
       Hours of Operation (Test ME-13)	11
  8    Top and Bottom Views of Mist Eliminator After 213
       Hours of Operation (Test ME-1^)	13
  9    Top and Bottom Views of Mist Eliminator After 500
       Hours of Operation (Test ME-15)	13
 10    Side, Top, and Bottom Views of Mist Eliminator
       After 1000 Hours of Operation (Test ME-15)	lU
 11    Side View of Mist Eliminator After 13l»-
       Hours of Operation (Test ME-17)	15
 12    Side, Top, and Bottom Views of Mist Eliminator
       After 560 Hours of Operation (Test ME-18)	17
 13    Trends in Operating Data	18

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INTRODUCTION

TVA has operated the 1-MW wet lime/limestone pilot plant at the Colbert
Steam Plant since February 1971.  Until recently, this pilot plant was
used primarily for testing limestone scrubbing with major attention
directed toward the full-scale 550-MW Widows Creek limestone scrubbing
system.

Results from this testing suggested utilizing a vertical mist eliminator
in a horizontal duct.  This type of mist elimination design permits the
use of a separate wash system for the mist eliminator than that of the
scrubber.  More recently, the pilot plant tests were designed to evaluate
similar methods for washing this type of mist eliminator without exceed-
ing the water balance of the closed-loop limestone wet scrubbing process.
The quantity of fresh water required for effective washing of the mist
eliminator on a once-through basis was four to five times the amount
required for makeup to the closed-loop slurry system.  One such method
of maintaining continuous operation of the mist eliminator in the hori-
zontal duct while operating in a closed-loop slurry system is the use of
sodium carbonate in the recyclable mist eliminator wash system.  This
additive increases the solubility of sulfates thus reducing the tendency
for scale formation.  The additive method may not be applicable for
washing the mist eliminator in the vertical duct because of the difficulty
in separating the wash liquor from the scrubber liquor.  Such separation
is necessary to avoid loss of sodium carbonate which would be prohibi-
tively expensive.

The major objective of the current study is to develop reliable closed-
loop mist eliminator washing techniques for lime/limestone systems where
the mist eliminator is positioned in the vertical duct.  This report
covers the systematic operation of a Chevron-type mist eliminator leading
to its 1000 hour long-term run in the limestone mode and 560 hour run in
the lime mode.
                                    1

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SUMMA.RY AND CONCLUSIONS

Pilot-plant tests have demonstrated washing methods that maintain
continuous mist eliminator performance.  Continuous performance of
a horizontally mounted mist eliminator operating in the limestone
mode is difficult because the wash water required for proper
washing cannot be separated from the slurry system.  Closed-loop
operation precludes using copious amounts of fresh water to main-
tain reliable mist eliminator performance since the allowable
makeup water rate is approximately 0.7 gpm or 0.2 gpm/ft  of duct
area.  The recommended wash rate is 5 gpm/ft .  An intermittent
wash using additional sources of wash liquor had to be used.

Washing the mist eliminator intermittently in the limestone mode
with fresh makeup water was not successful.  This may partly be
attributed to operating the limestone mode at a stoichiometry of
1.5.  Operation at this stoichiometry increases the plugging poten-
tial with soft mud-like solids due to excess limestone in the
scrubbing slurry being entrained into the mist eliminator.  The
accumulation was at such a rate that another liquid source was
needed to wash the mist eliminator.  The clarified liquor to the
scrubber system was accumulated and used to wash the mist elimin-
ator along with the allowable amount of makeup water.  Previous
testing has shown that washing the mist eliminator with a blend of
clarified liquor and makeup water results in chemical scaling and
plugging.  This chemical scale occurs when the supersaturated
clarified liquor reacts with the remaining SOg in the flue gas,
thus, resulting in the deposition of calcium-sulfur salts on the
mist eliminator blades.  Washing with clarified liquor followed by
makeup water was successful in removing the soft mud-like solids
and the calcium-sulfur salts from the mist eliminator.  Continuous

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mist eliminator performance in the limestone mode was maintained
by washing the bottom of the mist eliminator intermittently with
all the available clarified liquor immediately follo'wed by an
allocated amount of the allowable makeup water.  The top of the
mist eliminator was washed intermittently with the remaining
allocation of allowable makeup water.

Washing the mist eliminator intermittently in the lime mode with
fresh makeup water was successful.  The lime system operated at a
stoichiometry of 1.0 which alleviated having excess alkali material
in the scrubbing slurry being entrained into the mist eliminator.
Continuous mist eliminator performance in the lime mode was main-
tained by washing the bottom of the mist eliminator intermittently
with an allocated amount of allowable makeup water.  The remainder
of the allocated makeup water was used to wash the top of the mist
eliminator intermittently.  Proper implimentation of the available
wash water and the wash frequency is the key contributor in main-
taining continuous mist eliminator performance.  These results do
not say that all mist eliminator problems are solved, but the pro-
gress in that direction is certainly encouraging.

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WOEK COMPLETED
The pilot plant operated on a closed-loop basis.   The only liquor
purged from the system was that contained in the  discarded spent
solids (filter cake).  The quantity of liquor amounted to about
lUo pounds per hour when the filter cake contained 60 to 65 percent
solids.   Figure 1 shows  a flow diagram of the pilot plant, while
operating in the limestone mode.  Fredonia limestone (75% - 200
mesh)  was fed to the system at a rate sufficient  to maintain a
Ca:S02 mole ratio of 1.5 based on the concentration of S0_ in the
inlet  flue gas.  Scrubbing slurry containing 15 percent suspended
solids and 1.3 percent dissolved solids was  recirculated to the
venturi and absorber at  a liquid-to-gas ratio (L/G) of 10 and 50
gallons per 1000 cubic feet, respectively.   The scrubber contained
two stages (each 12 in deep) of 10-gram thermoplastic rubber (TPR)
spheres manufactured by  Moldcraft.
             REHEAT SYSTEM
               
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                           FIGURE 2
                CHEVRON  MIST ELIMINATOR
The Turbulent Contact Absorber (TCA)  operated at a superficial
velocity of 12.6 to 13.8 feet per second.   The concentration of
SOp in the inlet flue gas varied from about 1600 to 2700 ppm.  The
SOp removal averaged 72 percent.   This low SOg removal is attri-
buted to the absorber inlet spray header being lowered (approxi-
mately 15 ft) to just beneath the third grid so that  the mist
eliminator could be installed between the  third and fifth grids.
The particulate loading in the inlet and outlet averaged k.5 and
0.02 grains per standard cubic foot,  respectively.  The pressure
drop across the venturi and TCA-type absorber  (containing 3 grids
and 2 stages of the TPR spheres)  averaged  9 and 7 inches of water,
respectively.  The mist eliminator tested  was  the three-pass, 90-
degree bend, Chevron-type with 1-|- in spacings as shown in Figure
2.  The mist eliminator was placed in the  horizontal  position in
the vertical absorber tower.  Figure 3 shows the test module for
viewing the operation of the mist eliminator.

The initial run was designed to observe drainage and  mist entrain-
ment from the mist eliminator washes at superficial gas velocities
of 5, 7.5, 10. 12.6, and l6 ft/s using only air and water.   Proper

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drainage of the mist  eliminator occurred at 12.6 ft/s—the  planned
operating velocity.

The operation and washing conditions for all runs with the  mist
eliminator positioned in the vertical tower are summarized  in
Table 1.

Run ME-10 began on July 29, 19755 using flue gas and limestone
slurry with an initial pressure drop across the mist eliminator
of 0.2 inch HO.  The mist eliminator was washed intermittently
with only fresh makeup water--0.7 gal/min or 336 gal/shift.  Two-
thirds of this water  was used to wash the bottom of the mist
eliminator at one-hour intervals.  The remainder of the water
washed the top of the mist eliminator every two hours.  The
pressure drop gradually increased and leveled off several times
                             FIGURE 3
               MIST  ELIMINATOR TEST MODULE
                                 t

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                                                Top Wash
                                                                                    TABLE 1
                                                                      SUMMARY OF MIST ELIMINATOR OPERATIONS
                                                                                              Bottom Wash
Duration AP Pressure Rate Duration
Run of Test (in. H^O) (psi) (gpm) (min)
ME-9 12 h
ME-10 202 h 0.2—1.5 10 8 3.5
ME-ll 120 h 0.1—0.5 10 8.2 1.6
ME-12 96 h 0.1—0.2 10 8.2 1.6
ME-13 8U h 0.1— 0. U 10 8.2 1.6
ME-ll* 213 h 0.1—0.2 10 8.2 1.6
Interval Type Pressure
(h) Wash (psi)
2 FW 20
2 FW 20
2 FW 20
20
2 FW 20
20
2 FW 20
20
Rate
. (gjom) _
11.7
11.7
11.7
11.7
11.1*
11.1*
11.1*
11.1*
Duration
(min)
2.1*
1.5
1.8
1.53
1.8
1.53
1.55
Interval
1
0.5
0.5
0.5
0.5
0.5
0.5
0.5
Type Total ME Wai
Wash (gal/shift)

FW
FW
CL*
FW
CL*
FW
CL*
FW

337
333
337
339
328
332
985
335
jh
Comments
Air/water test.
Top two passes clean.
Lower lip plugged with mud-like deposits
Top two pases clean. Lower lip
plugged with mud-like deposits
with indications of scale in mud.
Top two passes clean. Bottom center
plugged probably due to spray pattern.
Used 2 nozzles at 5.7 gpm. Suddenly
started plugging. Upset unknown.
Similar to ME-13. May begin having
problems maintaining solids
ME-15   1000 h     0.1—0.1      10      8.2      1.6
ME-16    166 h     0.1—0.2      10      8.2
                                                   1.6
ME-17    131* h     0.1—0.2      10      8.2      1.6


ME-18    560 h     0.1 — 0.1      10      8.2      1.6
FW:  Fresh makeup water 0.7 gpm:  336 gal/shift
CL:  Clarified liquor
SL:  Slurry
20
20
15
20
15
20
11.1*
11.1*
6.0
ll.U
6.0
11.1*
2.7
0.78
2.7
0.78
2.7
0.78
0.25
0.25
0.25
0.25
0.25
0.25
CL*
FW
SL*
Fit
SL*
FW
985
338
518
338
518
338
                                                                        FW
                                                                                 20
U.I*
          0.65
                                                                                                             0.25
                                        289
  concentration.  May have been
  stopped premature—one small area
  causing pluggage—rest clean with
  little mud on bottom edges
  (always there).

Nozzles were raised to cover a missed
  area 9-9-75.  ME momentarily removed
  after 500 hours for photographing.
  Units 3,1*, and 5 off-line—pilot
  plant shut down 10-6 to 10-8.  ME
  remained clean through 1,000 hours.

Second pass plugging.  Nozzles plugging
  and cleaned by blast of air (30 psi)--
  may have helped clean ME.
  Nozzles eroded.

Separate and rotating slurry header.
Plugging in second pass.

Lime mode:  0.6 gpm makeup--288 gal/shift
  ME remained clean while using only
  fresh makeup water
•Followed imnediated with fresh water wash

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                                                                 •f *
                                  7,'.
                             FIGURE 4
       TOP  AND  BOTTOM  VIEWS OF  MIST ELIMINATOR
      AFTER 202 HOURS OF OPERATION (TEST  ME-10)


before the run was terminated  at a pressure drop of 1.5  inches
HO.  The run lasted  approximately 200 hours.  During this  run,
the top two passes remained  clean indicating a sufficient,  if not
excessive, top wash.   The  bottom pass was plugged with soft, mud-
like deposits mainly  on  the  lower lip of the mist eliminator.
Figure k shows the accumulation of this material on the  mist
eliminator.  It was decided  that a pressure drop of 1.5  inches
HO was excessive  as  a terminating point--no stopping point had
been determined up to this point.  A more realistic termination
point of 0.5-inch  HO was  selected for the next run.

Run ME-11 began on August  6, 1975, with an initial pressure drop
of 0.1 inch HpO.  Since  the  top passes remained clean during the
previous run, half of the  makeup water used to wash these passes
was added to the bottom  wash.  The frequency of the bottom  wash
was reduced to every  30  minutes.  The pressure drop rose slowly
until reaching the termination point after about 120 hours.
Figure 5 shows the appearance  of the mist eliminator at  the end of
this run.  Its appearance  was  similar to that in the previous run.
The lower lip was  partially  plugged with soft solids, but there
                               :

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                            FIGURE 5
      TOP  AND  BOTTOM  VIEWS OF  MIST ELIMINATOR
     AFTER  120 HOURS OF OPERATION  (TEST ME-II)
were indications  of scale deposits in this mud.   The scale forma-
tion was probably due  to the remaining S0? in the flue gas reacting
with soft solids  already attached to the mist eliminator thus
forming the hard  calcium sulfate salts.  From experience at
Colbert and Shawnee and from calculations on pressure drop versus
percent pluggage  of the mist eliminator, a pressure drop increase
of 0.1-in HpO when starting at 0.1-in HpO gives  a 30 percent
pluggage.  Therefore,  a new termination point of 0.2-in HpO was
chosen for all subsequent runs.
Run ME-12 began on August 10, 1975, with an initial pressure drop
of 0.1-in HpO.   Since  the top two passes remained clean during the
previous run and reducing more water from this  wash to add to the
bottom wash would be an almost insignificant addition, some of the
available clarified liquor was used to supplement the bottom wash.
Previous mist eliminator tests, prior to this project, had indi-
cated that washing with a mixture of clarified  liquor--saturated
with CaSOi—and fresh  water would result in scale formation on
the blades.  With this experience, it was decided to use clarified

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                                  •
                           FIGURE  6
      SIDE AND  BOTTOM VIEWS  OF  MIST ELIMINATOR
      AFTER  96  HOURS  OF  OPERATION  (TEST  ME-12)
liquor as the bottom wash and to immediately follow this wash with
the fresh makeup water.  Such operation reduces the possibility of
any clarified liquor remaining on the blades for any length of
time and becoming supersaturated with CaSOi  and cause scaling to
occur.  The pressure drop during this run ronained fairly constant
for approximately 100 hours when the center of the lower lip be-
gan plugging thus causing termination of the run.  Figure 6 shows
the plugged area that caused the increase in pressure drop.  The
small area that had accumulated the soft deposits was believed to
be caused by an uneven distribution of the wash and additional
nozzles were recommended for subsequent runs.

Run ME-13 began on August 19, 19755 with an initial pressure drop
of 0.1-in HO.  Two nozzles were used for the bottom wash with a
total wash similar to the previous runs using one nozzle.  The
duration of the bottom wash was adjusted to account for the
difference while the top wash remained the same.  The pressure
drop remained constant for approximately 100 hours when it
suddenly rose to O.U-in HO.  The reason for this increase is not
certain.  Figure 7 shows the appearance of the mist eliminator at
                               10

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                          FIGURE  7
     SIDE  AND  BOTTOM  VIEWS OF MIST  ELIMINATOR
     AFTER  84 HOURS  OF OPERATION  (TEST ME-13)
the end of this  run.

Run ME-lU began  on August 23, 1975? with an initial pressure drop
of 0.1-in H_0.   It was decided to increase  the clarified liquor
wash to the maximum available--approximately 100 gal/shift or
three times that used previously.  The fresh makeup water wash
immediately followed this clarified liquor  wash.   There was some
concern about maintaining adequate solids concentration with the
addition of this clarified liquor.  However, the concentrations
were held fairly close to design conditions. After approximately
200 hours of operation, the run was terminated after reaching a
pressure drop of 0.2-in H?0.  This termination may have been pre-
mature because of the variability of the pressure  drop readings.
Figure 8 shows the accumulation of mud on the mist eliminator at
the end of this  run.
Run ME-15 began on September 1, 1975, with an initial pressure
drop of 0.1-in H_0.   The only difference between this run and the

                              11

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previous run is the frequency of the bottom wash was changed from
every 30 minutes to every 15 minutes.  The washing duration was
therefore adjusted to maintain the same total wash on the bottom.
The pressure drop of 0.1-in HO was maintained for 1000 hours.
The mist eliminator was momentarily removed after 500 hours for
photographing.  Figure 9 shows the appearance of the mist elimin-
ator at that time.  Figure 10 shows the appearance of the mist
eliminator after completion of the long-term run.

Run ME-16 began on October Ik, 1975, to test the effect of washing
the mist eliminator with absorber slurry and fresh makeup water.
An initial pressure drop across the mist eliminator was 0.1-in
HO.  The bottom of the mist eliminator was washed at 15-min
intervals with absorber slurry followed immediately by the major-
ity of the fresh makeup water.  The top wash remained the same.
A buildup of soft mud-like solids occurred in the second pass of
the mist eliminator.  More than likely, this buildup was caused
by an accumulation of slurry solids that were carried into the
mist eliminator during the slurry wash sequence.  The same header
was used for the slurry wash as the makeup water wash.  High-
pressure air was used frequently to dislodge slurry solids from
the two spray nozzles.  This resulted in a portion of the solids
which originally accumulated in the second pass to be blown into
the third pass where they were removed by the top wash.  The net
effect of using high-pressure air to aid in cleaning the mist
eliminator is uncertain.  After 166 hours of operation, the
pressure drop reached 0.2-in HO and the run was terminated.

Run ME-17 began on October 21, 1975» using the same washing
techniques as ME-16 with the exception that a separate spray
header with larger nozzles was used for the slurry wash.  These
nozzles plugged with slurry solids and high-pressure air was un-
successful to unplug these nozzles because a sufficient back
pressure could not be maintained.  The solids accumulated in the
second pass of the mist eliminator at a faster rate than the

                                12

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                      • VI
                 FIGURE  8
TOP  AND BOTTOM VIEWS OF MIST ELIMINATOR
AFTER  213 HOURS OF OPERATION (TEST ME-14)
                 FIGURE 9
TOP AND BOTTOM VIEWS OF MIST  ELIMINATOR
AFTER 500 HOURS OF OPERATION  (TEST ME-15)
                   13

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                    FIGURE 10
SIDE, TOP, AND  BOTTOM VIEWS OF MIST  ELIMINATOR
  AFTER  1000 HOURS OF OPERATION  (TEST ME-15)
                       11*

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                            FIGURE  II
              SIDE VIEW OF MIST  ELIMINATOR
     AFTER 134  HOURS  OF  OPERATION   (TEST ME-17)

previous run.   This may be due to the elimination of high-pressure
air hitting the mist eliminator.  The run was terminated after
13^- hours of operation when  the pressure drop reached 0.2-in H?0.
Figure 11 shows the spray headers and the mud deposits in the
second pass at the end of the run.

Run ME-18 began on November  29, 1975? using lime as the absorbent
in the scrubber.  The chemistry of the absorption of SO  is
different in the lime mode which results in higher utilization of
the absorbent and, therefore, a reduction in the amount of water
removed with the sludge.  The makeup water requirement for the
lime mode is approximately 0.6 gal/min/MW as compared to 0.7
gal/min/MW for limestone.  This reduces the quantity of water
available to wash  the mist eliminator.  As a base case the mist
eliminator was washed intermittently with fresh makeup water only.
The top was washed every 2 hours and the bottom every 15 minutes.
The pressure drop  across the mist eliminator remained 0.1-in HO
                               15

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through 560 hours of operation.  At that time, the pilot plant
was shut down for the Christmas holidays.  Figure 12 shows the
appearance of the mist eliminator at the end of the lime run.
This run completed the mist eliminator tests in the vertical duct.
Trends in operating data for all runs are graphically displayed
in Figure 13.
                                 16

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                    FIGURE  12
SIDE, TOP,  AND BOTTOM VIEWS OF MIST ELIMINATOR
  AFTER 560  HOURS OF OPERATION  (TEST ME-18)

                       17

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 SBtf
sill
Jfi
   a!"
      to>-
      13-
      U -
           CALS.I).
 n  ii  e  o
	ME-II    i
                                    I  I  •  I
                                    H  B  W  IT
 it 20 a
T40UTOFSERVKC-
                                                     t  I  '  '
                                                            Z72t»903l3I39 J4 M
                                                            	ME-K	J
                                     FIGURE  13
                          TRENDS  IN OPERATING DATA
                                        18

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.OS

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     a.
   — oe
  Ulk
   o
   S .06
   S -04
        -J	1	1
                                            J	L
     90-
     80-
     70-
     60 -
     50.
        J	1	1	I   I   I
                            -1	1	1	I   I   I
                                            J	I   I
 S*  90
        	CLEAR UOUOR RETURN
        	 ABSORBER SLURRY
                 i   i  i
                            I   I  i   I   I
  i   •**
  !?  *
  3.  J5
  h  JO
                            I   I  I   i   I   I
§ e 20
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    1.5
                                                                i  i   i	i
                                            I   I   I   I  I   I
                            -UNIT 3 OUT OF SERVICE
           I   i   i   i  i
                            i   i	I	1	1	L
                                            i   i   i   i  i   i   i
                                                               I   I	1	1	1	1
(OCT"
           23456789K>lll2l3
WI5l6r7l8l92O
        ME-16 -
                                                               2l2223242526
                                                                    ME-17 - ^
                             FIGURE  13  (CONT.)
                      TRENDS IN  OPERATING  DATA
                                       20

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   20 -
a   M
If  .0*1
   "r
   60-
   120 •
   110-
   100-
   90 -
   so -
   70 -
   60 -
   50 —
CLEAR LIQUOR RETURN
ABSORBER FEO
83 075
1  05
                                                             I   I  t
                                                             I   I  I
     (11-24-79)

    J	ME-17—»
                          9  10  II  12  13  H  13  B  17  18
                                                        21  22 23  24
                                                                       27  28 29
                                                                        (I2-21-T5I
                   ME-16
                            FIGURE  13  (CONT.)
                     TRENDS IN  OPERATING DATA
                                     21

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FUTURE WORK

The remaining task scheduled for this project is the development
of a high velocity scrubber and mist eliminator combination.  A
modified TCA scrubber, using lime as the absorbing media, will be
operated at a gas velocity of 16 ft/sec.  The Chevron mist elimin-
ator will be positioned horizontally in the vertical duct and will
initially be washed similarly to the previous lime runs.
                                22

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CONVERSION FACTORS



The Environmental Protection Agency policy is to express all

measurements in metric units.  Implementing this practice will

result in undue lack of clarity.  The following conversion factors

are provided to convert the nonmetric units to the International

System of Units (Si).
To Convert From

Inches HpO
          P
Pound/inch  (psi)

Pound (Ib)

Gallon/minute (gpm)

Gallon (gal)

Foot/second (ft/sec)

Foot2 (ft2)

Foot3 (ft3)
                         To

                         Millimeter Mercury (mm Hg)

                         Atmosphere (atm)

                         Kilogram (kg)

                         Liter/minute (1/min)

                         Liter (1)

                         Meter/second (m/sec)

                         Meter2 (m2)

                         Meter3 (m3)
Multiply By

1.868 x 10°

6.805 x 10"2

It.536 x 10"1

3.785 x 10°
3.785 x 10

3.CA-8 x 10

9.290 x 10
-1
-2
Degree Fahrenheit ( F)   Degree Centigrade ( C)
2.832 x 10"2

t  = (t, - 32)/1.8
                                   23

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                                    TECHNICAL REPORT DATA
                             (Please read Instructions on the reverse before completing)
 1. REPORT NO.
  EPA-600/7-76-021
             3. RECIPIENT'S ACCESSION-NO.
4. TITLE AND SUBTITLE
 TVA's 1-MW Pilot Plant:   Vertical Duct Mist Elimination
    Testing—Progress Report
             5. REPORT DATE
                October 1976
             6. PERFORMING ORGANIZATION CODE
7. AUTHOR(S)
            G. A. Hollinden, R. F. Retards, N0 D, Moore
  (TVA-Chatt), T. M.  Kelso,  and R. M. Cole (TVA-MShoals)
             8. PERFORMING ORGANIZATION REPORT NO.

                PRS-lU
9. PERFORMING ORGANIZATION NAME AND ADDRESS
 TVA, Power Research Staff, Chattanooga, TN  37^01
 and TVA, Office  of  Agricultural and Chemical Development,
   Muscle Shoals, AL  35660
              10. PROGRAM ELEMENT NO.
                EHB528
              11. CONTRACT/GRANT NO.

                EPA-IAG-D5-0721
 12. SPONSORING AGENCY NAME AND ADDRESS
 EPA, Office of Research and Development
 Industrial Environmental Research Laboratory
 Research Triangle Park, NC  27711
              13. TYPE OF REPORT AND PERIOD COVERED
                Progress Report: 6-12/75	
              14. SPONSORING AGENCY CODE

                EPA-ORD
 is. SUPPLEMENTARY NOTES  EPA prcg ect officer for this  report is John E. Williams, Mail
 Drop 61, Ext 2915.
 16. ABSTRACT
 The report reviews (for-both the lime and limestone  systems) the systematic test
 program which  developed recent TVA-demonstrated washing techniques that maintain
 continuous mist  eliminator performance for lime/limestone closed-loop scrubbing systems
 at TVA's 1-MW  pilot plant at the Colbert power plant.   Continuous operation of the
 chevron-type mist eliminator, positioned horizontally in a vertical duct, in the
 limestone system was maintained (after extensive  testing) by washing the bottom of the
 mist eliminator  intermittently with all the  available clarified liquor,  immediately
 followed by an allocated amount of the allowable  makeup water.  The top of the mist
 eliminator was washed intermittently with the remaining allocation of allowable
 makeup water.  Continuous mist eliminator performance in the lime system was maintained
 by washing the bottom of the mist eliminator intermittently with an allocated amount
 of allowable makeup water.  The remainder of the  allocated makeup water was used to
 wash the top of  the mist eliminator intermittently.
17.
                                 KEY WORDS AND DOCUMENT ANALYSIS
                   DESCRIPTORS
                                               b.lDENTIFIERS/OPEN ENDED TERMS  C. COSATI Field/Group
 Air Pollution
 Scrubbers
 Washing
 Calcium Oxides
 Limestone
 Air Pollution Control
 Stationary Sources
 Mist Eliminators
 13B
 07A
 13H
 07B
18. DISTRIBUTION STATEMENT
   Unlimited
19. SECURITY CLASS (ThisReport}
 Unclassified
21. NO. OF PAGES
  29-
20. SECURITY CLASS (Thispage)
 Unclassified
                                                                          22. PRICE
EPA Form 2220-1 (9-73)

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