' P A U'S' Environmental Protection Agency Industrial Environmental Research       EPA~600/7-78~051d
"•  »» Office of Research and Development  Laboratory                       jft-re
                         Research Triangle Park. North Carolina 27711 MBTCn 1978
               EPA UTILITY FGD SURVEY:
               December 1977 - January 1978
               Interagency
               Energy-Environment
               Research and Development
               Program Report

-------
                 RESEARCH REPORTING SERIES


Research reports of the Office of Research and Development, U.S. Environmental
Protection Agency, have been grouped into nine series. These nine broad cate-
gories were established to facilitate further development and application of en-
vironmental technology. Elimination  of traditional  grouping  was consciously
planned to foster technology transfer and a maximum interface in related fields.
The nine series are:

    1. Environmental Health Effects Research

    2. Environmental Protection Technology

    3. Ecological Research

    4. Environmental Monitoring

    5. Socioeconomic Environmental Studies

    6. Scientific and Technical Assessment Reports  (STAR)

    7. Interagency Energy-Environment Research and Development

    8. "Special" Reports

    9. Miscellaneous Reports

This report has been  assigned to the INTERAGENCY ENERGY-ENVIRONMENT
RESEARCH AND  DEVELOPMENT series. Reports in this series result from the
effort funded  under the 17-agency Federal Energy/Environment Research and
Development Program. These studies relate to EPA's mission to protect the public
health and welfare from adverse effects of pollutants associated with energy sys-
tems. The goal of the Program is to assure the rapid development of domestic
energy supplies in an environmentally-compatible manner by providing the nec-
essary environmental data and control technology. Investigations include analy-
ses of the transport of energy-related pollutants and their health and ecological
effects;  assessments  of, and development of, control technologies for energy
systems; and integrated assessments of a wide range of energy-related environ-
mental issues.
                        EPA REVIEW NOTICE
This report has been reviewed by the participating Federal Agencies, and approved
for publication. Approval does not signify that the contents necessarily reflect
the views and policies of the Government, nor does mention of trade names or
commercial products constitute endorsement or recommendation for use.

This document is available to the public through the National Technical Informa-
tion Service, Springfield, Virginia 22161.

-------
                                   EPA-600/7-78-051a
                                           March 1978
  EPA UTILITY  FGD SURVEY:
December 1977 - January 1978
                     by

               Bernard A. Laseke, Jr.

              PEDCo Environmental, Inc.
                11499 Chester Road
               Cincinnati, Ohio 45246
               Contract No. 68-01-4147
                    Task 3
             Program Element No. EHE624
                EPA Project Officers:
              N. Kaplan and J. C. Herlihy

        Industrial Environmental Research Laboratory
          Office of Energy, Minerals and Industry
           Research Triangle Park, N.C. 27711
                  Prepared for

       U.S. ENVIRONMENTAL PROTECTION AGENCY
           Office of Research and Development
               Washington, D.C. 20460

-------
                             NOTICE
     This report, (prepared by PEDCo Environmental, Inc.,
Cincinnati, Ohio under EPA Contract No. 68-01-4147, Task No. 5)
is provided as an information transfer document.  Data in this
report are supplied voluntarily by utility representatives; flue
gas desulfurization (FGD) system designers, vendors, and sup-
pliers; regulatory personnel; and others.  Neither EPA nor the
designated contractor warrants the accuracy or completeness of
information contained in this report.

     The format of this report, which represents the first in a
series of six, has been extensively revised from previous issues.
The succeeding five issues will be supplemental in nature.  The
user is therefore cautioned to retain this issue for reference
throughout the year, because much of the inf_or_inat.io_n, contained in.
this_ report will not be published again untjA around March 1979.
Supplemental issues wTTl be cumulative, so that it will be
necessary only to retain the latest issue and this report to have
all available information.

     Initial distribution of the report (generally, one copy per
company) is limited to organizations and individuals indicating a
specific interest in the field of FGD technology.  Additional
copies of this report and succeeding issues can be purchased from
National Technical Information Service, Springfield, Virginia
22151.
                               ii

-------
                         CONTENTS
Notice                                                      ii
Tables                                                      iv
Executive Summary and Highlights                             v
Table 1  Summary List of FGD Systems                         1
Table 2  Status of FGD Systems                                4
Table 3  Performance Description for Operational FGD Systems   22
Table 4  Summary of FGD Systems by Company                 146
Table 5  Summary of FGD Systems by Vendor                  147
Table 6  Summary of New and Retrofit FGD Systems by Process  149
Table 7  Summary of Operating FGD Systems by Process and
        Generating Units                                    150
Table 8  Summary of Sludge Disposal Practices for Operational
        FGD Systems                                       151
Table 9  Summary of FGD Systems by Process and Regulatory
        Class                                              152
Table 10 Summary of FGD Systems Under Construction          154
Table 11 Summary of Planned  FGD Systems                    156
Table 12 FGD System Operations That Have Been Terminated
        or Shut Down Indefinitely                             159
Table 13 Total of FGD Megawatt Capacity by Year               213
Appendix A   FGD Systems Economics                        A-l
Appendix B   FGD Process Flow Diagrams                    B-l
Appendix C   Definitions                                    C-l
                            iii

-------
                             TABLES

Number                                                Page

   I  Number and Total MW of FGD Systems                v

  II  Summary of Changes: FGD Summary Report, December
     1977 - January 1978                                 ix

  IE  Performance of Operational Units During December -
     January Period                                     x
                               iv

-------
                EXECUTIVE SUMMARY AND HIGHLIGHTS
This report is prepared every other month by PEDCo Environmental,
Inc., under a contract to the Industrial Environmental Research
Laboratory/RTF and the Division of Stationary Source Enforcement
of the U.S. Environmental Protection Agency.  Table 1 summarizes
the current status of the FGD systems addressed in this two-month
period.

                           Table I

               NUMBER AND TOTAL MW OF FGD SYSTEMS
Status
Operational
Under construction
Planning:
Contract awarded
Letter of intent
Requesting/evaluating bids
Considering only FGD systems
TOTAL
No. of
units
31
38

20
3
6
33
131
MW
10,550
15,664

10,415
865
2,660
15,525
55,679
Table II  (page vii) summarizes the individual units that changed
status during the report period.

The performance of the operating systems is summarized in Table
III (page viii).  Other activity highlights during the months of
December and January are summarized below:

Present total power-generating capacity in the United States is
approximately 570,000 MW.  Of this total 250,000 MW are generated
by coal.  As indicated in Table I, 31 FGD-equipped units, repre-
senting 10,550 MW of power capacity, are now in service. - Thus, a
little under 2 percent of the total capacity and a little over 4

-------
percent of the coal-fired capacity are controlled by FGD.  By
1986 the projected total power-generating capacity in the United
States will be 800,000 MW.  Of this total approximately 570,000
MW will be coal-fired.  As indicated in Table I, 131 FGD-equipped
units representing 55,679 MW are projected for service.  There-
fore, assuming that no unit retirements occur, about 7 percent of
the total projected generating capacity and about 16 percent of
the projected coal-fired capacity will be controlled by FGD in
1986.

Alabama Electric Cooperative reported that construction of the
Tombigbee 3 limestone FGD system commenced during the period.
Foundation work is now in progress.

Arizona Public Service reported that Cholla 1 was not in service
during the latter part of November, all of December, and the
first part of January because of a scheduled unit outage for
turbine, boiler, and FGD system overhaul.  The unit resumed
operations in late January and the boiler operated 135 hours
during the remainder of the month.  The A and B FGD modules
operated 131 and 123 hours in January, producing operability
index values of 97 and 91 percent, respectively.

Cincinnati Gas & Electric announced that the FGD contract for
East Bend 2 has been awarded to Babcock & Wilcox  (B&W).  B&W will
design and supply a lime scrubbing FGD system which will go into
operation in January 1981.

Columbus and Southern Ohio Electric reported that the A-module of
the Conesville 5 FGD system was restarted on December 3, 1977.
The A-module operated 162 hours with an availability of 93
percent.  The B-module operated 199 hours in December with an
availability of 97 percent.  Conesville 5 was shut down for a
scheduled 3-month turbine, boiler, and FGD system overhaul
beginning December 12, 1977.

Indianapolis Power & Light Company declared Petersburg 3 com-
mercial on November 29 with two of its four scrubber modules in
operation.  All four modules were certified operable in December
prior to a scheduled outage for completion of heat tracing.

Kansas City Power & Light Company reported that La Cygne 1 had a
total system availability of 94 percent in November and 97 per-
cent in December.  The unit operated only 300 hours in December
because of a turbine overhaul.

The Department of Electric and Water Utilities of the City of
Lakeland, Florida, is currently evaluating bids for a new 350-MW
coal-fired power-generating unit scheduled for installation at
their Mclntosh Station.  Mclntosh 3 will fire 2.5 to 3.0 percent
sulfur coal and utilize ESP's and an FGD system for particulate

-------
and sulfur dioxide control.  Mclntosh 3 is scheduled for opera-
tion in October 1981.

The PGD system on the 178-MW Cane Run 4 of Louisville Gas &
Electric  (LG&E) was available 85 and 90 percent for December and
January, respectively.  Although the utility encountered lime
feed freeze up problems, the FGD system itself experienced no
problems that required outage time during the period.  LG&E also
reported that the Mill Creek 4 FGD system is now under construc-
tion.

Montana Power reported that the Colstrip 1 and 2 lime/alkaline
flyash FGD systems were available 96 and 98 percent, respec-
tively, in December, and 98 percent for both systems in January.

Nevada Power reported operability index values for the Reid
Gardner 3 FGD system of 92 and 99 percent for December and
January, respectively.  The Reid Gardner 2 FGD system remained in
service during the period.  The Reid Gardner 3 FGD system was
down throughout December for repairs to the booster fan (new wear
plates).

Northern States Power reported that the Sherburne No. 1 FGD
system was available 93 percent during the period.  The No. 2 FGD
system was available 93 percent in December and 92 percent in
January.  Unavailability of the No. 1 system was attributed
primarily to heavy maintenance on the 107 module.  Unavailability
of the No. 2 system was attributed to strainer and wash screen
replacement in the module reaction tanks which commenced in late
December and continued throughout the period.

Otter Tail Power announced that a -contract has been awarded to
Wheelebrator-Frye and Atomics International  (AI) for a sodium
carbonate FGD system for Coyote No. 1.  The FGD system combines
AI's aqueous carbonate process in a fabric filter supplied by
Wheelebrator-Frye.  The 400-MW system is scheduled to start-up
in May 1981.

Pacific Gas & Electric  (PG&E) announced that it plans to install
a 2-unit, coal-fired power-generating station in Northern Cali-
fornia.  PG&E plans to burn low sulfur coal  (0.8 percent) in both
800-MW units and use ESP's and FGD systems for the control of
particulates and sulfur dioxide.  Tentative operation dates are
1984 and 1985.

Potomac Electric and Power  (PEPCO) reported that S02-removal
capability will not be included in the wet scrubber modules now
being installed on Dickerson 1 and 2.  PEPCO plans to meet state
emission regulations by burning low or medium sulfur coal in
these units.
                               VI 1

-------
Public Service of Indiana  (PSI) announced that the FGD systems
planned for Gibson 3 and 4 have been cancelled because of a
recent district court decision identifying the units as existing
sources.  PSI also announced that an FGD system is being planned
for Gibson 5, which is a new coal-fired unit scheduled for opera-
tion in 1982.

The Tennessee Valley Authority reported that the 530-MW Widows
Creek 8 FGD system achieved an operability of 97 percent in
December and 96 percent in January.  In addition, TVA also
announced that the FGD contract for the Widows Creek 7 was
awarded to Combustion Engineering  (CE).  CE will design and
supply a 575-MW limestone  scrubbing spray tower system for this
unit.
                               VI 1 1

-------
TABLE II.   SUMMARY OF CHANGES:  FGD SUMMARY  REPORT,  DECEMBER 1977-JANUARY  1978
FGD status report
11/30/77
Alabama Electric coop.
Tomb ig bee No. 3
Cincinnati Gas b Electric
East Bend No. 2
Cofnoonwealth Edison
Will County No. 1
De Ima r va Powe r
Lakeland Dept. of Elec. b Water
Mclntoah, No . 3
Lou 13 vi 1 le Gas b Electric
Hill Creek No. 4
Ot ter Ta 1 1 Power
Coyote No. 1
Pacific Gaa b Electric
Fossil No. 1
Paci f ic Gas b Electric
Fossil No. 2
Potomac Electric b Power
Dickerson No . 1
Potomac Electric b Power
Dickerson No. 2
Gibson 3
Gibson 4
Gibson 5
Tennessee Valley Authority
Widows Creek No. 7
United Power Association
Coal Creek 1
Wisconsin Power b Light
Columbia No. 2
1/31/78
Operational
No.
32





-1























31
MW
10,717





167























10,550
Under
No.
34

tl








tl















tl


38
MW
14,219

225








495




Cont rdct
awarded
No.
20

-1

+ 1






-1

tl













545


15,664






tl

-1

tl
20
MW
9,758

225

600






495

400











575

545

527
10,415
Letter of
No .
4




























-1
3
MW
1,392




























527
865
Requesting/
No.
fl



-1




Cons ider my
FGD
MW NO.
4,210



600


34






MW
14,630








tl , 350












-1
-1






6










650
650






2,660




-1






400

tl 800

tl 800

-1 190

-1 190


tl
-1




33


650
575




15,525
Total
No.
132





-1


*!





tl

tl

-1

-1
-1
-1
tl





131
MW
54,926





167


350





800

800

190

190
650
650
650





55,679

-------
            TABLE  III.    PERFORMANCE  OF  OPERATIONAL  UNITS


                        DURING  DECEMBER-JANUARY  PERIOD
Plant
Cholla 1
Cone s\ 1 1 le 5
Elrama
Phil lips
Petersburg 3
Hawthorn 3
Hawthorn 4
La Cygne 1
Lawrence 4
Lawrence 5
Green River
1. 2. and 3
Cane Run 4
Paddys Run 6
M. R. Young 2
Colstrip 1
Colstrip 2
Reid Gardner 1
Reid Gardner 2
Reid Gardner 3
D.H. Mitchell 11
Sherburne 1
Sherburne 2
Bruce
Mansfield 1
Bruce
Mansfield 2
Eday stone 1A
Winyah 2
Southwest 1
Shawnee IDA
Shawnee 10B
Widow's Creek 8
Martin LaXe 1
Total (31)

capacity
115
400
510
410
530
140
100
820
125
400
64
178
65
450
360
360
125
125
125
115
710
710
825
825
120
280
200
10
10
550
793
10,550
PCD unit
period*
115
400
310
410
530
140
100
820
125
400
64
178

450
360
360
125
125
125
115
710
710


120
280

10
10
550
793
8,435
No
period

















825
825







1.650
Shut down
period


200







65










200




465
FGD lyaten
Dec-

95



73
70
97

50
85


98
98
85
0
88

93
93


41"




56


Jan





47
68
94

"
90



56
67
99

92
92







18


FGD ayitem
opera-
bili ty
Dec

69







63
85



32
0
92










97


1 1) " •
Jan









32
67



68
74
99










96


FGD •yaterr
Dec

72







63
100



33
0
96










59


Jan
94








32
87



69
67
99










96


FGD ayatem
< 1 )
Dec

24







50
82



71
0
93










56


Jan









23
67



56
67
99










79


 • This category  include! the flue gaa capacity being handled by the FGD eyete« at l«a»t part of the tine during
  the report period.

•• The percent figure* lilted are average values for all •yatem «crubbing train* during the period in question.

a Cuiwnulative  (October, November, December)

-------
  FGO STATUS REPORT 01/78

    COMPANY NAME
                                          TABLE 1
                               SUMMARY LIST OF FGO SYSTEMS
                                         UNIT NAME
                                  START UP DATE   STATUS
                                                                                           REG
                                                                                           CLASS
   ALABAMA ELECTRIC COOP
   ALABAMA ELECTRIC COOP
   ALLEGHENY POWER SYSTEM
   ALLEGHENY POWER SYSTEM
   ARIZONA ELECTRIC POWER COOP
   ARIZONA ELECTRIC POWER COOP
   ARIZONA PUBLIC SERVICE
   ARIZONA PUBLIC SERVICE
   ARIZONA PUBLIC SERVICE
   ARIZONA PUBLIC SERVICE
   ARIZONA PUBLIC SERVICE
   ARIZONA PUBLIC SERVICE
   ARIZONA PUBLIC SERVICE
   ARIZONA PUBLIC SERVICE
   BASIN ELECTRIC POWER COOP
   BASIN ELECTRIC POWER COOP
   BASIN ELECTRIC POWER COOP
   BASIN ELECTRIC POWER COOP
   BASIN ELECTRIC POWER COOP
   BIG RIVERS ELECTRIC COOP CORP.
   BIG RIVERS ELECTRIC COOP CORP.
   BOARD OF MUNICIPAL UTILITIES
   BRAZOS ELECTRIC POWER COOP
   CENTRAL ILLINOIS LIGHT CO.
   CENTRAL ILLINOIS LIGHT CO.
   CENTRAL ILLINOIS PUBLIC SERV
   CENTRAL MAINE POWER CO.
   CINCINNATI GAS & ELECTRIC CO.
   COLORADO UTE ELECTRIC ASSN.
   COLORADO UTE ELECTRIC ASSN.
   COLUMBUS & SOUTHERN OHIO ELEC.
   COLUMBUS & SOUTHERN OHIO ELEC.
   COLUMBUS & SOUTHERN OHIO ELEC.
   COLUMBUS & SOUTHERN OHIO ELEC.
   COMMONWEALTH EDISON
   DELMARVA POWER CO.
   DUQUESNE LIGHT
   DUOUESNE LIGHT
   EASTERN KENTUCKY POWER COOP
   GENERAL PUBLIC UTILITIES
   GENERAL PUBLIC UTILITIES
   GULF POWER CO.
   GULF POWER CO.
   GULF POWER CO.
   HOOSIER COOPERATIVE
   HOOSIER COOPERATIVE
   INDIANAPOLIS POWER » LIGHT CO.
   INDIANAPOLIS POWER & LIGHT CO.
   KANSAS CITY POWER & LIGHT
   KANSAS CITY POWER & LIGHT
   KANSAS CITY POWER & LIGHT
   KANSAS POWER & LIGHT
   KANSAS POWER & LIGHT
   KANSAS POWER & LIGHT
   KANSAS POWER & LIGHT
   KENTUCKY UTILITIES
   LAKELAND UTILITIES
   LOUISVILLE GAS & ELECTRIC
   LOUISVILLE GAS & ELECTRIC
  TOMBIGBEE NO.  2                     6-78
  TOMBIGBEE NO.  3                     6-79
  PLEASANTS NO.  i                     3-79
  PLEASANTS NO.  a                     3-eo
  APACHE NO a                         6-78
  APACHE NO 3                         4-79
  CHOLLA NO 1                        10-73
  CHOLLA NO a                         6-78
  CHOLLA NO. 4                        6-80
  FOUR CORNERS NO. 1                   0-  0
  FOUR CORNERS NO. 2                   0-0
  FOUR CORNERS NO. 3                   0-0
  FOUR CORNERS NO. 4                   0-0
  FOUR CORNERS NO. 5                   0-0
  ANTELOPE VALLEY NO. 1                0-81
  ANTELOPE VALLEY NO. 2                0-83
  LARAMIE RIVER  NO. 1                 4-80
  LARAMIE RIVER  NO. a                10-80
  LARAMIE RIVER  NO. 3                 6-83
  REID NO. 3                         12-79
  REID NO. 3                         13-80
  SIKESTON POWER STATION             11-80
  SAN MIGUEL NO. 1                   13-79
  DUCK CREEK NO. 1                    8-78
  DUCK CREEK NO.a                     1-83
  NEWTON NO.l                        11-79
  SEARS ISLAND NO. 1                  11-86
  EAST BEND NO 2                      1-81
  CRAIG NO. 1                         3-79
  CRAIG NO. 2                         3-79
  CONESVILLE NO  5                     1-77
  CONESVILLE NO  6                    10-78
  POSTON NO. 5                        0-81
  POSTON NO. 6                        0-83
  POWERTON NO. 51                    ia-79
  DELAWARE CITY  NOS.  1   2 &  3         4-80
  ELRAMA POWER STATION                10-75
  PHILLIPS POWER STATION              7-73
  SPURLOCK GENERATING PLANT  NO.i.       3-80
  COHO NO.l                           5-87
  SEWARD NO.7                         5-84
  CRIST NO. 4 AND NO. 5                0-76
  CRIST NO. 6 AND NO. 7                0-80
  LANSING SMITH  NO. 1 AND NO. Z        0-80
  MEROM NO. 1                         0-80
  MEROM NO. a                         o-ai
  PETERSBURG NO  3                    10-77
  PETERSBURG NO  4                     4-82
  HAWTHORN NO, 3                     ll-7a
  HAWTHORN NO. 4                      8-72
  LA CYGNE NO 1                        2-73
  JEFFERY NO. 1                        6-78
  JEFFERY NO. 2                        6-80
  LAWRENCE NO 4                       ia-68
  LAWRENCE NO 5                       11-71
  GREEN RIVER NOS. 1   3   AND 3        9-75
  MCINTOSH POWER PLANT  UNIT  NO.3      10-81
  CANE RUN NO 4                        8-76
  CANE RUN NO 5                        4-78
2
a
z
2
2
a
i
2
3
6
6
6
6
6
6
6
3
3
6
2
2
3
2
2
6
a
6
3
a
a
i
2
6
6
2
2
1
1
5
7
7
7
7
7
5
5
1
5
1
1
1
2
2
1
1
1
5
1
2
A
A
A
A
B
B
B
B
E
B
B
B
B
B
B
B
B
B
B
A
A
A
A
A
A
A
A
A
B
B
B
B
6
B
C
C
3
6
A
A
A
B
B
B
A
A
A
A
B
B
C
B
B
B
B
C
A
B
B
1.  OPERATIONAL UNITS
2.  UNITS UNDER CONSTRUCTION
3.  PLANNED - CONTRACT AWARDED
4.  PLANNED - LETTER OF INTENT SIGNED
5.  PLANNED - REQUESTING/EVALUATING BIDS
6.  CONSIDERING ONLY FGD SYSTEMS
7.  CONSIDERING FGD SYSTEMS AS WELL AS ALTERNATIVE METHODS
A.  BOILER CONSTRUCTED SUBJECT TO FEDERAL NSPS
B.  BOILER SUBJECT TO STATE STANDARD THAT IS MORE STRINGENT THAN THE FEDERAL NSPS
C.  BOILER SUBJECT TO STATE STANDARD THAT IS EQUAL TO OR LESS STRINGENT THAN NSPS
D.  OTHER
E.  REGULATORY CLASS UNKNOWN

-------
  FGO STATUS REPORT 01/78

    COMPANY NAME
                                          TABLE 1
                               SUMMARY LIST OF FGD SYSTEMS
                                         UNIT NAME
                                                                  START UP DATE   STATUS
                                                           REG
                                                           CLASS
   LOUISVILLE GAS & ELECTRIC
   LOUISVILLE GAS & ELECTRIC
   LOUISVILLE GAS & ELECTRIC
   LOUISVILLE GAS & ELECTRIC
   LOUISVILLE GAS & ELECTRIC
   LOUISVILLE GAS & ELECTRIC
   MINNESOTA POWER AND LIGHT CO.
   MINNKOTA POWER COOPERATIVE
   MONTANA POWER CO.
   MONTANA POWER CO.
   MONTANA POWER CO.
   MONTANA POWER CO.
   NEVADA POWER
   NEVADA POWER
   NEVADA POWER
   NEVADA POWER
   NEVADA POWER
   NEVADA POWER
   NEVADA POWER
   NEVADA POWER
   NEVADA POWER
   NEVADA POWER
   NEW ENGLAND ELEC SYSTEM
   NIAGARA MOHAWK POWER COOP.
   NORTHERN  INDIANA PUB SERVICE
   NORTHERN  INDIANA PUB SERVICE
   NORTHERN  INDIANA PUB SERVICE
   NORTHERN  STATES POWER CO.
   NORTHERN  STATES POWER CO.
   NORTHERN  STATES POWER CO.
   NORTHERN  STATES POWER CO.
   OTTER  TAIL POWER COMPANY
   PACIFIC GAS AND ELECTRIC
   PACIFIC GAS AND ELECTRIC
   PACIFIC POWER AND LIGHT CO.
   PENNSYLVANIA POWER CO.
   PENNSYLVANIA POWER CO.
   PENNSYLVANIA POWER CO.
   PHILADELPHIA ELECTRIC CO.
   PHILADELPHIA ELECTRIC CO.
   PHILADELPHIA ELECTRIC CO.
   PHILADELPHIA ELECTRIC CO.
   POTOMAC ELECTRIC & POWER
   POWER  AUTHORITY OF NEW YORK
   PUBLIC SERVICE CO OF NEW MEX.
   PUBLIC SERVICE CO OF NEW M£X.
   PUBLIC SERVICE CO OF NEW HEX.
   PUBLIC SERVICE CO OF NEW HEX.
   PUBLIC SERVICE OF INDIANA
   SALT RIVER PROJECT
   SALT RIVER PROJECT
   SALT RIVER PROJECT
   SOUTH  CAROLINA PUBLIC SERVICE
   SOUTH  CAROLINA PUBLIC SERVICE
   SOUTHERN  ILLINOIS POWER COOP
   SOUTHERN  INDIANA GAS&ELECTHIC
   SOUTHERN  MISSISSIPPI ELECTRIC
   SOUTHERN  MISSISSIPPI ELECTRIC
   SPRINGFIELD CITY UTILITIES

1.  OPERATIONAL UNITS
2.  UNITS UNDER CONSTRUCTION
3.  PLANNED  - CONTRACT AWARDED
  CANE RUN NO 6
  MILL CREEK NO 1
  MILL CREEK NO ^
  MILL CREEK NO 3
  MILL CREEK NO 4
  PADDYS RUN NO 6
  CLAY BOSWELL NO. 4
  MILTON R. YOUNG NO. 2
  COLSTRIP NO 1
  COLSTHIP NO 2
  COLSTRIP NO. 3
  COLSTRIP NO. 4
  HARRY ALLEN STATION NO. 1
  HARRY ALLEN STATION NO. ^
  HARRY ALLEN STATION NO. 3
  HARRY ALLEN STATION NO. «
  REID GARDNER NO 1
  REID GARDNER NO Z
  REID GARDNER NO 3
  REID GARDNER NO 4
  WARNER VALLEY STATION NO.  1
  WARNER VALLEY STATION NO.  2
  BRAYTON POINT NO.3
  CHARLES R. HUNTLEY NO.6
  BAILLY NO. 7
  BAILLY NO. 8
  D.H. MITCHELL NO.11
  SHEHBURNE COUNTY STATION NO.l
  SHERBURNE COUNTY STATION NO.2
  SHERBURNE COUNTY STATION NO.3
  SHERBURNE COUNTY STATION NO.4
  COYOTE NO. 1
  FOSSIL NO. 1
  FOSSIL NO. 2
  JIM BHIDGEH NO. 4
  SRUCE MANSFIELD NO. 1
  BRUCE MANSFIELD NO. 2
  BRUCE MANSFIELD NO. 3
  CROMBY
  EDDYSTONE NO. IA
  EDOYSTONE NO. IB
  EDDYSTONE NO. 2
  DICKERSON NO. 0
  ARTHUR KILL
  SAN JUAN NO. 1
  SAM JUAN NO. £
  SAN JUAN NO. 3
  SAN JUAN NO. 4
  GIBSON 5
  CORONADO NO.l
  CORONADO NO.2
  CORONAOO NO.3
  WINYAH NO. 2
  WJNYAH NO. 3
  MARION NO. 4
  A.B. BROWN NO.l
  R.D. MOHROW NO.l
  R.O. MORROW NO.2
  SOUTHWEST NO. 1
11-79
 1-82
 1-81
 4-78
 6-80
 4-73
 0-80
 9-77
11-75
 7-76
 7-80
 7-81
 6-63
 6-84
 6-85
 6-86
 4-74
 4-74
 7-76
 0- 0
 6-82
 6-63
 0- 0
 0-80
 0- 0
 0- 0
 6-77
 3-76
 4-77
 5-81
 5-83
 5-81
 0-84
 0-85
 9-79
 4-76
 7-77
 4-80
 6-80
 9-75
 6-60
 6-80
 5-85
 9-62
 4-78
 7-78
 1-79
 5-81
 0-82
 4-79
 4-80
 0-97
 7-77
 0-80
 6-78
 4-79
 5-78
 8-78
 4-77
2
6
6
2
2
1
3
1
1
1
3
3
6
6.
6
6
1
1
1
4
6
6
6
3
6
6
1
1
1
3
3
3
6
6
2
1
1
3
b
1
4
6
7
7
2
2
4
6
b
3
3
6
1
5
2
2
2
2
1
B
B
B
B
A
C
A
B
B
8
B
B
B
B
8
B
8
a
B
B
B
B
C
C
C
C
C
B
B
B
B
B
B
B
B
B
B
B
B
B
B
B
D
B
8
B
6
B
A
B
B
B
A
A
A
A
A
A
A
4.  PLANNED - LETTER OF INTENT SIGNED
5.  PLANNED - REQUESTING/EVALUATING BIDS
6.  CONSIDERING ONLY FGD SYSTEMS
7.  CONSIDERING FGD SYSTEMS AS WELL AS ALTERNATIVE METHODS
A.  BOILER CONSTRUCTED SUBJECT TO FEOtRAL NSPS
B.  BOILER SUBJECT TO STATE STANDARD THAT IS MOKE STRINGENT THAN THE FEDERAL NSPS
C.  BOILER SUBJECT TO STATE STANDARD THAT IS EQUAL TO OR LESS STRINGENT THAN NSPS
D.  OTHER
E.  REGULATORY CLASS UNKNOWN

-------
 FGD STATUS REPORT 01/78

   COMPANY NAME
                                         TABLE  1
                               SUMMARY  LIST OF FGD  SYSTEMS
                                         UNIT  NAME
                                                                  START UP DATE    STATUS
                      REG
                      CLASS
  SPRINGFIELD  WATER   LIGHT&POWER
  TENNESSEE  VALLEY  AUTHORITY
  TENNESSEE  VALLEY  AUTHORITY
  TENNESSEE  VALLEY  AUTHORITY
  TENNESSEE  VALLEY  AUTHORITY
  TEXAS  MUNICIPAL  POWER  AGENCY
  TEXAS  POWER  AND  LIGHT  CO.
  TEXAS  POWER  AND  LIGHT  CO.
  TEXAS  POWER  AND  LIGHT  CO.
  TEXAS  UTILITIES  CO.
  TEXAS  UTILITIES  CO.
  TEXAS  UTILITIES  CO.
  TEXAS  UTILITIES  CO.
  TEXAS  UTILITIES  CO.
  TEXAS  UTILITIES  CO.
  UNITED POWER ASSOCIATION
  UNITED POWER ASSOCIATION
  UTAH POWER & LIGHT CO.
  UTAH POWER & LIGHT CO.
  VIRGINIA ELECTRIC AND  POWER CO
  WISCONSIN POWER  & LIGHT CO.
                                  DALLMAN  NO.  3
                                  SHAWNEE  N0.10A
                                  SHAWNEE  NO.108
                                  WIDOWS CREEK NO.  7
                                  WIDOWS CREEK NO.  8
                                  GIBBONS  CREEK UNIT  NO.
                                  SANDOW NO.4
                                  TWIN  OAKS  NO. 1
                                  TWIN  OAKS  NO. 2
                                  FOREST GROVE NO.  1
                                  MARTIN LAKE  NO.  1
                                  MARTIN LAKE  NO.  2
                                  MARTIN LAKE  NO.  3
                                  MARTIN LAKE  NO.  
-------
 COMPANY

 POWER STATION
                     TABLE  2
          STATUS  OF  FGD  SYSTEMS AS OF
                                        01/78
                                                          CURRENT  MONTH
ALABAMA ELECTRIC COOP
TOMBIGBEE NO. 2
  225  MW - NEW
COAL 0.8 - 1.5 PERCENT SULFUR
PEABODY ENGINEERING
LIMESTONE SCRUBBING
STARTUP   6/78
       PEABOOY  ENGINEERING  HAS BEEN AWARDED THE CONTRACT FOR THE INSTALLATION
       OF  A  LIMESTONE  SCRUBBING SYSTEM ON THIS UNIT.  A HIGH-EFFICIENCY ESP WILL
       BE  INSTALLED  UPSTREAM  OF THE SCRUBBING  SYSTEM  TO PROVIDE PRIMARY
       PARTICULATE CONTROL.  THE FGD SYSTEM CONTAINS TWO SCRUBBING TRAINS,
       TREATING APPROXIMATELY  70 PERCENT  OF THE FLUE  GAS FUR REMOVAL OF SULFUR
       DIOXIDE. STACK  GAS  REHEAT WILL  NOT 8E REQUIRED. THE TOTAL INSTALLED COST
       FOR BOTH TOMBIGBEE  NO.  2 AND NU.  3 FGD  SYSTEMS IS $40.46 MM. CURRENTLY,
       ERECTION OF THE SCRUBBING EQUIPMENT IS  IN PROGRESS.
ALABAMA ELECTRIC COOP
TOMBIGBEE NO. 3
  225  MW - NEW
COAL 0.8 - 1.5 PERCENT SULFUR
PfcABODY ENGINEERING
LIMESTONE SCRUBBING
STARTUP   6/79
       PEABODY  ENGINEERING  HAS  BEEN AWARDED  THE  CONTRACT FOR THE INSTALLATION
       OF  A  LIMESTONE  SCRUBBING SYSTEM ON  THIS  UNIT.  A  HIGH-EFFICIENCY ESP WILL
       BE  INSTALLED  UPSTREAM  OF THE SCRUBBING  SYSTEM  TO PROVIDE PRIMARY
       PARTICULATE  CONTROL.  THE FGD SYSTEM CONTAINS TWO SCRUBBING TRAINS,
       TREATING APPROXIMATELY 70 PERCENT  OF  THE  FLUE  GAS FOR REMOVAL OF SULFUR
       DIOXIDE. STACK  GAS  REHEAT WILL  NOT  BE REQUIRED.  UNIT NO. 3 TURBINE AND
       BOILER  ARE  CURRENTLY  UNDER CONSTRUCTION.  CURRENTLY,  FOUNDATION WORK ON
       THE SCRUBBER  PLANT  IS  COMPLETE. EQUIPMENT ERECTION WILL COMMENCE SHORTLY.
 ALLEGHENY  POWER  SYSTEM
 PLEASANTS  NO.  i
  625  MW  -  NEW
 COAL 4.5 PERCENT  SULFUR
 BABCOCK &  WILCOX
 LIME SCRUBBING
 STARTUP    3/79
       THE  THREE  PRINCIPAL  OPERATING  UTILITY  COMPANIES OF  THE ALLEGHENY HOWF.R
       SYSTEM ARE INSTALLING AN EMISSION CONTROL SYSTEM FOR THIS NEW COAL-FIRED
       UNIT  WHICH INCLUDES  A HIGH  EFFICIENCY  ESP UPSTREAM  OF FOUR TRAY TOWERS
(MAX)   FOR  THE  CONTROL  OF  PARTICULATES  AND  SULFUR DIOXIDE.  DESIGN REMOVAL
       EFFICIENCIES  FOR THIS EMISSION CONTROL SYSTEM ARE 99.5 AND 90 PERCENT
       RESPECTIVELY.  THE ORAVO CO.  IS SUPPLYING THIOSORBIC  LIME. THE CONSULTING
       ENGINEERING FIRM IS  UNITED  ENGINEERS AND CONSTRUCTORS. CURRENTLY, EREC-
       TION  OF  THE SCRUBBING EQUIPMENT  IS IN  PROGRESS.
 ALLEGHENY  POWER  SYSTEM
 PLEASANTS  NO.  2
   625   MW  -  NEW
 COAL 1.5 PERCENT  SULFUR  (MAX)
 BABCOCK &  WILCOX
 LIME SCRUBBING
 STARTUP    3/80
       THE THREE  PRINCIPAL OPERATING  UTILITY  COMPANIES OF THE ALLEGHENY POWER
       SYSTEM ARE INSTALLING AN EMISSION CONTROL SYSTEM FUR THIS NEW COAL-FIRtD
       UNIT WHICH INCLUDES A HIGH EFFICIENCY  ESP UPSTREAM OF FOUR TRAY TOWERS
       FOR THE CONTROL OF  PARTICULATES AND SULFUR DIOXIDE. DESIGN REMOVAL
       EFFICIENCIES FOR THIS EMISSION CONTROL SYSTEM ARE 99.5 AND 90 PERCENT,
       RESPECTIVELY. THE DRAVO CO. IS SUPPLYING THIOSORBIC LIME. THE CONSULTING
       ENGINEERING FIRM IS UNITED ENGINEERS AND CONSTRUCTORS. CURRENTLY,  FOUNDA-
       TION WORK  ON THE SCRUBBER PLANT IS IN  PROGRESS.
 ARIZONA  ELECTRIC  POWER  COOP
 APACHE  NO  3
   200   MW  -  NEW
 COAL  0.5- 0.8 PERCENT  SULFUR
 RESEARCH COTTRELL
 LIMESTONE  SCRUBBING
 STARTUP    6/78
       AEPC HAS AWARDED A CONTRACT TO RESEARCH COTTRELL FOR A WET LIMESTONE
       SCRUBBING SYSTEM. THE UNIT WILL FIRE BITUMINOUS COAL WITH A SULFUR CON-
       TENT OF 0.5-0.8X, AND ASH CONTENT OF 10.OX (HEATING VALUE - 10,000-
       11,000 BTU/LB).  THERE is A 22 ACRE SLUDGE POND AND A 64 ACRE ASH POND.
       PONDS WILL BE UNLINED AND 10 FEET DEEP. THERE WILL BE NO REHEAT. CON-
       STRUCTION OF  THE SYSTEM IS NOW NEARING COMPLETION. ALL FGD EQUIPMENT IS
       INSTALLED. SCRUBBER LINING IS COMPLETE. THE PLASTIC GIRDERS SUPPORTING
       THE MIST ELIMINATORS WERE REPLACED WITH STEEL GIRDERS.
 ARIZONA  ELECTRIC  POWER  COOP     STRUCTURAL  STEELWORK  FOR  HOT-SIDE  UOP  ESP'S  is  COMPLETE.  STRUCTURE
 APACHE  NO  3                     ERECTION  OF  THE  SCRUBBER-ABSORBER  TOWERS  IS  COMPLETE.  EACH SCRUBBER CAN
   200   MW  -  NEW                 HANDLE  400,000  ACFM  3 270  F  AND  RECIRCULATE  20,000  GPM OF SLURRY.  BOILER
 COAL    0.5-  0.8  PERCENT SULFUR  CONSTRUCTION HAS BEGUN.  THERE  ARE  CURRENTLY  2  PONDS WITH  A TOTAL OF 20-
 RESEARCH COTTRELL              YRS  CAPACITY FOR THE  DISPOSAL  OF THE  UNFIXATED  SLUDGE. 2  ADDITIONAL PONDS
 LIMESTONE  SCRUBBING             ARE  PLANNED  PROVIDING AN  ADDITIONAL 20 YRS  OF  DISPOSAL CAPABILITY. THERE
 STARTUP    4/79                  WILL BE NO  REHEAT  AND A  KELLOGG  LINER  IS  PLANNED  FOR THE  WET STACK, WHICH
                                WILL CONSIST OF  A  COMMON  OUTER SHELL  AND  A  SEPARATE FLUE  FOR EACH  UNIT.
 ARIZONA  PUBLIC  SERVICE
 CHOLLA  NO  1
   115   MW  -  RETROFIT
 COAL    0.44-1 PERCENT SULFUR
 RESEARCH COTTRELL
 LIMESTONE  SCRUBBING
 STARTUP  10/73
       REFER TO THE BACKGROUND INFORMATION SECTION IN TABLE 3 OF THIS REPORT.
       THIS LIMESTONE SCRUBBING SYSTEM WAS PLACED IN SERVICE IN OCTOBER 1973.
       THE SCRUBBER PLANT CONSISTS Of TWO PARALLEL SCRUBBING TRAINS. PARTICU-
       LATE CONTROL IS PROVIDED BY TWO FLOODED-DISC SCRUBBERS. S02 CONTROL IS
       PROVIDED BY ONE PACKED (MUNTERS PACKING) TOWER (A-SIDE). FLUE GAS CLEAN-
       ING WASTES ARE DISCHARGED TO AN EXISTING FLY ASH POND. NO WATER IS RE-
       CYCLED BACK FROM THE DISPOSAL POND. IN-LINE STEAM HEHEATEHS RAISE THE
       GAS TEMPERATURE 40 F.
 ARIZONA  PUBLIC  SERVICE
 CHOLLA NO  2
   250  MW  -  NEW
 COAL   0.14-1 PERCENT SULFUR
 RESEARCH COTTRELL
 LIMESTONE  SCRUBBING
 STARTUP    6/78
       THE CONTRACT FOR THIS WET LIMESTONE SCRUBBING SYSTEM HAS BEEN AWARDED
       BY THE UTILITY TO RESEARCH-COTTRELL.  THIS SYSTEM IS A LARGER-SCALE
       APPLICATION OF THE CHOLLA NO.l DESIGN. ALL DESIGN AND ENGINEERING WORK
       HAVE BEEN COMPLETED. CONSTRUCTION OF  THE UNIT IS NOW NEARING COMPLETION.
       THE UNIT COMMERCIAL START-UP DATE IS  JUNE 1978. THE FGD SYSTEMANT
       CONSISTS OF FOUR PARALLEL FLOOOED-DISC SCRUBBERS AND PACKED TOWER ABSORBER
       TRAINS. THREE ARE REQUIRED FOR FULL LOAD CAPACITY. INITIAL BOILER START-
       UP DATE IS FEBRUARY 1978.

-------
 COMPANY

 POWER STATION
              TABLE 2
   STATUS OF F60 SYSTEMS AS OF   01/76

                          CURRENT MONTH
ARIZONA PUBLIC SERVICE
CHOLLA NO. 4
  350  MW - NEW
COAL  0.44-1 PERCENT SULFUR
RESEARCH COTTRELL
LIMESTONE SCRUBBING
STARTUP   6/80
UNIT NO. 4 IS CURRENTLY UNDER CONSTRUCTION. APS HAS AWARDED THE F6D CON-
TRACT TO RESEARCH COTTRELL. THE STATE REGULATORY AGENCY HAS NOT YET DE-
CIDED THE EMISSIONS REGULATIONS WHICH WILL APPLY TO THE PLANT. THE C-E
BOILER WILL FIRE THE SAME COAL AS CHOLLA NO. 1, WITH SULFUH CONTENT OF
0.44-1.0 PERCENT. THE A-E FIRM IS EBASCO. COMMERCIAL START-UP IS SLATED
FOR 06/80. THE FGD SYSTEM IS A DOUBLE LOOP LIMESTONE ABSORPTION PROCESS
AND REVENUES OF THE CONTRACT TO R-C ARE REPORTED TO BE S5 MM.
ARIZONA PUBLIC SERVICE
FOUR CORNERS NO.  1
  175  MW - RETROFIT
COAL 0.75 PERCENT SULFUR
CHEMICO/APS
LIME/ALKALINE FLYASH  SCRUBBING
STARTUP   O/ 0
 ARIZONA PUBLIC  SERVICE
 FOUR CORNERS NO. 2
   175  MW - RETROFIT
 COAL 0.75 PERCENT SULFUR
 CHEMICO/APS
 LIME/ALKALINE FLYASH  SCRUBBING
 STARTUP   O/ 0
 ARIZONA PUBLIC  SERVICE
 FOUR CORNERS  NO.  3
   229  MW - RETROFIT
 COAL 0.75 PERCENT SULFUR
 CHEMICO/APS
 LIME/ALKALINE FLYASH  SCRUBBING
 STARTUP   O/  0
 ARIZONA  PUBLIC  SERVICE
 FOUR  CORNERS  NO.  4
   755 MW  - RETROFIT
 COAL  0.7 PERCENT  SULFUR
 NOT SELECTED
 NOT SELECTED
 STARTUP    O/  0
APS MAY BE UPGRADING THE OPERATIONAL PARTICULATE SCRUBBERS AT THE FOUR
CORNERS UNIT NOS. 1, 2 AND 3 FOR 802 REMOVAL. EACH UNIT HAS 2 VENTURI
SCRUBBER MODULES FOR PARTICULATE CONTROL. APPROXIMATELY 30X OF THE FLUE
GAS S02 CONTENT IS REMOVED AT THE PRESENT TIME IN THE VENTURIES BECAUSE
OF THE ALKALINITY OF THE COLLECTED FLYASH. NEW MEXICO APC OFFICIALS  IN-
DICATED THAT THE FOUR CORNERS STATION WILL BE REQUIRED TO REDUCE S02
EMISSIONS AT LEAST 67.5* OF THE CURRENT LEVEL. UPGRADING OF THE VENTURIES
WOULD BE AFFECTED BY SUPPLEMENTING THE ALKALINITY OF THE SCRUBBING FLUID.

APS MAY BE UPGRADING THE OPERATIONAL PARTICULATE SCRUBBERS AT THE FOUR
CORNERS UNIT NOS. 1, 2 AND 3 FOR S02 REMOVAL. EACH UNIT HAS 2 VENTURI
SCRUBBER MODULES FOR PARTICULATE CONTROL. ROUGHLY 30X OF THE FLUE GAS S02
CONTENT is REMOVED AT THE PRESENT TIME IN THE VENTURIES WITH THE HIGH
ALKALINE FLYASH. NEW MEXICO APC OFFICIALS INDICATED THAT THE 5 FOUK  COR-
NERS UNITS WILL BE REQUIRED TO REMOVE AT LEAST 67.5X OF THE S02 CONSIDER-
ING ALL OF THE PLANTS TOGETHER. UPGRADING OF THE VENTURIES WOULD BE  AF-
FECTED BY ADJUSTING ACID-ALKALINITY.

APS MAY BE UPGRADING THE OPERATIONAL PARTICULATE SCRUBBERS AT THE FOUR
CORNERS UNIT NOS. 1, 2 AND 3 FOR S02 REMOVAL. EACH UNIT HAS 2 VENTURI
SCRUBBER MODULES FOR PARTICULATE CONTROL. ROUGHLY 30X OF THE FLUE GAS S02
CONTENT IS REMOVED AT THE PRESENT TIME IN THE VENTURIES WITH THE HIGH
ALKALINE FLYASH. NEW MEXICO APC OFFICIALS INDICATED THAT THE 5 FOUR  COR-
NERS UNITS WILL BE REQUIRED TO REMOVE AT LEAST 67.5X OF THE S02 CONSIDER-
ING ALL OF THE PLANTS TOGETHER. UPGRADING OF THE VENTURIES WOULD BE  AF-
FECTED BY ADJUSTING ACID-ALKALINITY.

THE UTILITY IS CURRENTLY EVALUATING THE DATA AND INFORMATION ACCUMULATED
DURING THE HORIZONTAL PROTOTYPE SCRUBBING PROGRAM IN ORDER TO ASCERTAIN
VARIOUS POSSIBLE STRATEGIES TO CONTROL THE EMISSIONS FROM THIS COAL  FIRED
755-MW UNIT. APS MAY BE REQUIRED TO REDUCE THE CURRENT LEVEL OF 802  EMIS-
SIONS FROM THE ENTIRE PLANT BY 67.5X. A DECISION ON THE USE OF FGD FOR
THIS UNIT WILL BE ANNOUNCED SHORTLY.
 ARIZONA  PUBLIC  SERVICE
 FOUR  CORNERS  NO.  5
   755 MW  - RETROFIT
 COAL  0.7 PERCENT  SULFUR
 NOT SELECTED
 NOT SELECTED
 STARTUP    O/  0
THE UTILITY IS CURRENTLY EVALUATING THE DATA AND INFORMATION
ACCUMULATED DURING THE HORIZONTAL PROTOTYPE SCRUBBING PROGRAM
IN ORDER TO ASCEHTAIN VARIOUS POSSIBLE STRATEGIES TO CONTROL
THE EMISSIONS FROM THIS COAL-FIRED 755-MW UNIT. A DECISION,
PENDING THE OUTCOME OF LOCAL REGULATORY AGENCY HEARINGS
WILL BE ANNOUNCED IN THE NEAR FUTURE.
 BASIN  ELECTRIC  POWER  COOP
 ANTELOPE  VALLEY  NO. 1
   450  MW - NEW
 LIGNITE 1.0 PERCENT SULFUR
 NOT SELECTED
 NOT SELECTED
 STARTUP   0/81
THE UTILITY IS CURRENTLY PLANNING TO INSTALL A WET SCRUBBING SYSTEM TO
CONTROL S02 EMISSIONS FROM THIS LIGNITE-FIRED BOILER. VARIOUS PROCESSES
ARE NOW BEING EVALUATED BY THE UTILITY. THIS NEW FACILITY IS
LOCATED IN THE MERCER COUNTY AREA NEAR BEULAH, NORTH DAKOTA AND IS
KNOWN AS THE ANTELOPE VALLEY STATION. BOTH UNITS 1 AND 2 WILL BE REQUIRED
TO COMPLY WITH AIR EMISSION STANDARDS VIA BEST AVAILABLE TECHNOLOGY.
START-UP IS SCHEDULED FOR 1981. BIDS ARE EXPECTED TO GO OUT THIS SPRING.
 BASIN ELECTRIC POWER COOP
 ANTELOPE  VALLEY NO. 2
   450  MW - NEW
 LIGNITE 1.0 PERCENT SULFUR
 NOT SELECTED
 NOT SELECTED
 STARTUP   0/83
THE UTILITY IS CURRENTLY INVESTIGATING VARIOUS FGD PROCESSES FOR THIS
SECOND LIGNITE-FIRED UNIT SCHEDULED AT THIS NEW STATION LOCATED IN MERCER
COUNTY, NEAR BEULAH, NORTH DAKOTA. THIS NEW FACILITY WILL BE KNOWN AS
THE ANTELOPE VALLEY STATION AND WILL BE REQUIRED TO COMPLY WITH AIR
EMISSION STANDARDS VIA THE BEST AVAILABLE TECHNOLOGY. START-UP IS NOW
SCHEDULED FOR 1963. BIDS ARE EXPECTED TO GO OUT THIS SPRING.

-------
 COMPANY

 POWER STATION
                                             TABLE £
                                  STATUS  OF  FGD SYSTEMS AS OF
                                                                01/78
                                                         CURRENT MONTH
BASIN ELECTRIC POWER COOP
LARAMIE RIVER NO. 1
  550  MW - NEW
COAL  0.6 PERCENT SULFUR
RESEARCH COTTRELL
LIMESTONE SCRUBBING
STARTUP   4/80
                               RESEARCH-COTTRELL IS CURRENTLY FABRICATING THE DUAL-LOOP LIMESTONE WET
                               SCRUBBERS.  ON-SITE CONSTRUCTION IS TO BEGIN APRIL 1978. SLUDGE WILL BE
                               DEWATERED TO 83X SOLIDS BEFORE LANDFILL. THE SCRUBBERS WILL BE MADE OF
                               STAINLESS STEEL AND WILL HANDLE 2.3 MM ACFM AT 286 F. L/G RATIO WILL BE
                               60.  THE TOTAL CAPITAL COST FOR BOTH THE SYSTEMS IS ESTIMATED TO BE 80
                               MM DOLLARS. THE OPERATING COST WILL BE 1.5 MILLS/KWH. B*W HAS BEEN AWARD'
                               ED CONTRACT FOR 2 ESP'S AT A COMBINED COST OF $28 MM. THE ESP'S ARE FOR
                               UNITS 1 AND 2.  STACK WILL BE CONCRETE WITH ACID BRICK LINING.
BASIN ELECTRIC POWER COOP
LARAMIE RIVER NO. 2
  550  MW • NEW
COAL  0.8 PERCENT SULFUR
RESEARCH COTTRELL
LIMESTONE SCRUBBING
STARTUP  10/80
                               RESEARCH-COTTRELL IS CURRENTLY  FABRICATING THE DUAL-LOOP LIMESTONE WET
                               SCRUBBERS.  ON-SITE CONSTRUCTION IS TO BEGIN APRIL 1978. SLUDGE WILL BE
                               DEWATERED TO 63X SOLIDS BEFORE  LANDFILL.  THE SCRUBBERS WILL BE MADE OF
                               STAINLESS STEEL AND WILL HANDLE 2.3 MM ACFM AT 286 F. L/G RATIO  WILL BE
                               60.  THE TOTAL CAPITAL COST FOR  BOTH THE SYSTEMS IS ESTIMATED TO BE 80
                               MM DOLLARS.  THE OPERATING COST  WILL BE 1.5 MILLS/KWH. B&W HAS BEEN AWARD-
                               ED CONTRACT  FOR 2 ESP'S AT A  COMBINED COST OF $28 MM. THE ESP'S ARE FOR
                               UNITS 1 AND  2. STACK WILL BE  CONCRETE WITH ACID BRICK LINING.
BASIN ELECTRIC POWER COOP
LARAMIE RIVER NO.  3
  550  MW  -  NEW
COAL  0.8  PERCENT  SULFUR
NOT SELECTED
NOT SELECTED
STARTUP    6/83
                               THE UTILITY IS STILL CONSIDERING VARIOUS FGD PROCESSES. LARAMIE RIVER
                               STATION WILL FIRE SUB-BITUMINOUS COAL WITH THE FOLLOWING CHARACTERIS-
                               TICS* 8100 BTU/LB,  0.8 PERCENT SULFUR AND 7.0 PERCENT ASH.
                                THE  EMISSION CONTROL SYSTEM FOR THIS NEW COAL-FIRED  UNIT  IS  BEING  SUPP-
                                LIED BY  AMERICAN  AIR FILTER, THE SYSTEM WILL CONSIST  OF A  COLD-SIDE  ESP
                                AND  TWO  SPRAY  TOWERS CONTROLLING PARTICULATE AND  802  TO 99.6  PERCENT AND
                                90 PERCENT, RESPECTIVLEY. THE B&W BOILER WILL FIRE HIGH SULFUR  C3.5  TO
                                4.5  PERCENT) WESTERN KENTUCKY COAL. FGD SYSTEM FOUNDATIONS HAVE  BEEN
                                LAID,  ONE  REACTION  TANK  HAS BEEN ASSEMBLED AND A  SECOND TANK  IS  BEING
                                CONSTRUCTED. THE  FGD SYSTEM WILL INCLUDE AN INDIRECT  HOT  AIR  REHEAT  SYST.
                                IUCS WILL  CONSTRUCT A SLUDGE DISPOSAL SYSTEM TO SERVICE BOTH  REID  2  AND 3

                                THE  EMISSION CONTROL SYSTEM FOR THIS NEW COAL-FIRED  UNIT  IS  BEING  SUPP-
                                LIED BY  AMERICAN  AIR FILTER. THE SYSTEM WILL CONSIST  OF A  COLD-SIDE  ESP
                                AND  TWO  SPRAY  TOWERS CONTROLLING PARTICULATE AND  S02  TO 99.6  PERCENT AND
                                90 PERCENT, RESPECTIVELY. THE B&W BOILER WILL FIRE HIGH SULFUR  (3.5  TO
                                a.5  PERCENT) WESTERN KENTUCKY COAL. THE FGO SYSTEM WILL INCLUDE  AN
                                INDIRECT HOT AIR  REHEAT  SYSTEM. IUCS WILL CONSTRUCT  A  SLUDGE  DISPOSAL
                                SYSTEM TO  SERVICE BOTH REID 2 AND 3. THE BOILER IS CURRENTLY  UNDER CON-
                                STRUCTION.

                                B&W  WAS  AWARDED A CONTRACT FOR BOILER AND AIR QUALITY  CONTROL SYSTEM
                                INSTALLATION.  2.8 PERCENT SULFUR COAL IS TO BE BURNED. THE AOC  SYSTEM
                                WILL CONSIST OF 2 ESP'S  FOLLOWED BY 3 SCRUBBERS EACH  CAPABLE  OF  HANDLING
                                SOX  OF THE BOILER LOAD-ONE WILL BE ON STAND-BY AT ALL  TIMES.  SIKESTON
                                STATION  WILL FEATURE A DOUBLE-LINED STACK, 2 PONDS,  ONE FOR  FLY  ASH, THE
                                OTHER  FOR  SCRUBBER  SLUDGE/BOTTOM-ASH DISPOSAL, AND 4  AXIAL FLOW  FANS. NO
                                STACK  GAS  REHEAT  IS PLANNED. GROUND BREAKING IS SET  FOR APRIL 1978.  MAX-
                                IMUM FLUE  GAS  CAPACITY IS 748,390 ACFM $ 286 F.
BIG RIVERS ELECTRIC COOP CORP.
REID NO. 2
  250  MW - NEW
COAL 3.5-4.0 PERCENT SULFUR
AMERICAN AIR FILTER
LIME SCRUBBING
STARTUP  12/79
BIG RIVERS ELECTRIC COOP CORP.
REIO NO. 3
  240  MW - NEW
COAL 3.5-4.0 PERCENT SULFUR
AMERICAN AIR FILTER
LIME SCRUBBING
STARTUP  12/80
BOARD OF MUNICIPAL UTILITIES
SIKESTON POWER STATION
  235  MW - NEW
COAL 2.8 PERCENT SUFUR
BABCOCK & WILCOX
LIMESTONE SCRUBBING
STARTUP  11/80
 BRAZOS  ELECTRIC  POWER  COOP
 SAN  MIGUEL  NO.  1
   400   MW  - NEW
 LIGNITE 1.67  PERCENT SULFUR
 BABCOCK &  WILCOX
 LIMESTONE  SCRUBBING
 STARTUP  12/79
                               THE EMISSION CONTROL EQUIPMENT FOR THE COAL-FIKED RADIANT BOILER WILL
                               CONSIST OF AN ESP UPSTREAM OF FOUR LIMESTONE SCRUBBING MODULES.
                               THE SCRUBBER FLUE GAS CAPACITY IS NOMINALLY DESIGNED AT 1.579 MILLION
                               ACFM (302 F).  DESIGN S02 REMOVAL EFFICIENCY IS 86 PERCENT FOR 4aOO PPM
                               S02 INLET. L/G RATIOS ARE 10 AND 45 FOR QUENCHER AND ABSORBER, RESPEC-
                               TIVELY. RESEARCH COTTRELL HAS BEEN AWARDED SLUOGE DISPOSAL CONTRACT.
                               FGD SYSTEM FOUNDATION IS COMPLETE WITH STRUCTURAL STEEL SOON TO BE
                               ERECTED. BOILER CONSTRUCTION IS ABOUT 50* COMPLETE.
 CENTRAL  ILLINOIS  LIGHT  CO.
 DUCK  CREEK  NO.  1
   
-------
 COMPANY

 POWER STATION
              TABLE 2
   STATUS OF FGD SYSTEMS AS OF
       01/78

CURRENT MONTH
CENTRAL ILLINOIS LIGHT CO.
DUCK CREEK NO.2
  400  MM - NEW
COAL 2.5-3.0 PERCENT SULFUR
NOT SELECTED
LIMESTONE SCRUBBING
STARTUP   1/82
SCRUBBING UNIT IS SCHEUULEO TO COMMENCE OPERATIONS  IN JANUARY  1982. THE
UTILITY HAS NOT YET SELECTED A SYSTEM SUPPLIER. A DECISION CONCERNING
THE STATUS OF THE BOILER AND CONTROL STRATEGY WILL  BE ANNOUNCED  IN EARLY
1976. THE UTILITY IS LOOKING AT ESP'S FOR PARTICULATE CONTROL  AND
LIMESTONE OR DUAL ALKALI FOR S02 SCRUBBING. THE PLANT IS NOW IN  THE
PROCESS OF PREPARING SPECS.
CENTRAL ILLINOIS PUBLIC SERV
NEWTON NO.l
  575  MW - NEW
COAL 4.0 PERCENT SULFUR
BUELL/ENVIROTECH
DOUBLE ALKALI SCRUBBING
STARTUP  11/79
A CONTRACT HAS BEEN AWAROEO BY CIPSCO TO BUELL/ENVIROTECH FOR THE
INSTALLATION OF AN EMISSION CONTROL SYSTEM ON UMT NO. 1. THE KEY COM-
PONENTS OF THE EMISSION CONTROL SYSTEM INCLUDE* A HIGH-EFFICIENCY ESP,
FOUR PRECOOLERS, FOUR POLYSPHERE ABSORBERS, THKEE THICKENERS, TWO EX-
PERIMENTAL REHEAT SYSTEMS, AND THREE HORIZONTAL EXTRACTION FILTERS FOR
SLUDGE DEWATERING. APPROXIMATELY 25 PERCENT OF THE CONSTRUCTION WORK
AT THE PLANT HAS BEEN COMPLETED. THE FGD SYSTEM WILL HAVE CEILCOTE-
LINEO ABSORBER MODULES.
CENTRAL MAINE POWER CO.
SEARS  ISLAND NO.  1
  600  MW - NEW
COAL   SOURCE UNDETERMINED
NOT SELECTED
NOT SELECTED
STARTUP   11/86
BECAUSE OF THE DISCOVERY OF A GEOLOGICAL FAULT ON SEARS ISLAND, THE
UTILITY HAS CANCELLED PLANS FOR A 1150-MW NUCLEAR POWER PLANT. A
600-MW COAL-FIRED UNIT IS NOW BEING PLANNED IN ITS PLACE. COMMERCIAL
OPERATION IS PROJECTED FOR NOVEMBER 1986. COMPLIANCE WITH 302 NSPS WILL
BE ACHIEVED BY INSTALLING AN FGD SYSTEM. LIME AND LIMESTONE SCRUBBING
PROCESSES ARE BEING GIVEN PRIMARY CONSIDERATION. CURRENTLY, CMPCO HAS
FILED AN APPLICATION WITH THE STATE PUBLIC UTILITIES COMMISSION. AN EN-
VIRONMENTAL PERMIT APPLICATION WILL BE FILED WITHIN THE NEXT TWO YEARS..
 CINCINNATI GAS & ELECTRIC CO.
 EAST  BEND NO 2
   600   MW - NEW
 COAL
 BABCOCK  & WILCOX
 LIME  SCRUBBING
 STARTUP   1/81
A CONTRACT HAS BEEN CONDITIONALLY AWARDED TO BABCOCK AND WILCOX FOR A
COMMERCIAL LIME SCRUBBING SYSTEM. A COAL SOURCE AND SUPPLY HAS NOT BEEN
FINALIZED, COMMERCIAL START-UP DATE HAS BEEN DELAYED ONE YEAR TO JANUARY
1981. THE A-t DESIGN FIRM IS SARGENT AND LUNOY.
 COLORADO  UTE  ELECTRIC  ASSN.
 CRAIG  NO.  1
   450   MW  - NEW
 COAL 0.45  PERCENT  SULFUR
 PEABODY ENGINEERING
 LIMESTONE  SCRUBBING
 STARTUP    3/79
THE CONSTRUCTION OF THE LIMESTONE SLURRY SPRAY TOWER SCRUBBING
SYSTEM FOR SULFUR DIOXIDE REMOVAL FROM LOW-SULFUR COAL-FIRED BOILER FLUE
GAS HAS BEGUN. THE FOUNDATION IS COMPLETE AND THE SILOS ARE UP. PANTI-
CULATE CONTROL WILL BE PROVIDED BY HOT-SIDE ESP'S UPSTREAM OF THE SCRUB-
BER PLANT. SLUDGE DISPOSAL IS UNDECIDED. THERE WILL BE A STEAM COIL TYPE
STACK GAS REHEAT INCLUDED. REQUIRED PARTICULATE AND SULFUR DIOXIDE RE-
MOVAL EFFICIENCIES ARE 99.8 AND 85 PERCENT, RESPECTIVELY. FGD SYSTEM
START-UP IS SCHEDULED FOR SPRING 1979.
 COLORADO  UTE  ELECTRIC  ASSN.
 CRAIG  NO.  2
   450   MW  - NEW
 COAL 0.45  PERCENT  SULFUR
 PEABOOY ENGINEERING
 LIMESTONE  SCRUBBING
 STARTUP    3/79
PEABODY ENGINEERED SYSTEMS HAS BEEN AWARDED A CONTRACT IN EXCESS OF
$60 MILLION TO DESIGN AND SUPPLY A LIMESTONE SLURRY SPRAY TOWER
SCRUBBING SYSTEM FOR S02 REMOVAL FROM LOW-SULFUR COAL-FIRED BOILER FLUE
GAS FOR UNITS 1 & 2. PARTICULATE CONTROL WILL bE PROVIDED BY HOT-SIDE
ESP'S UPSTREAM OF THE SCRUBBER PLANT. SLUDGE WILL BE STABILIZED AND HAUL-
ED TO A MINE^ILL. THERE WILL BE A STEAM COIL TYPE STACK GAS REHEATER  IN-
CLUDED. REQUIRED PARTICULATE AND 502 REMOVAL EFFICIENCIES ARE 99.8
AND 85 PERCENT, RESPECTIVELY. FGD START-UP IS SCHEDULED FOR SPRING 1979.
 COLUMBUS  &  SOUTHERN  OHIO ELEC.
 CONESVILLE  NO  5
   400   MW -  NEW
 COAL 4.5  -  4.9 PERCENT  SULFUR
 UNIVERSAL OIL  PRODUCTS
 LIME SCRUBBING
 STARTUP   1/77
REFER TO THE BACKGROUND INFORMATION SECTION IN TABLE 3 OF  THIS REPORT.
THE BOILER AND ESP WERE COMPLETED AND PLACED IN SERVICE  IN SEPT.  1976.
THE B-SIDE MODULE BECAME AVAILABLE FOR SERVICE IN JANUARY  1977.
COMMERCIAL OPERATIONS WERE ACHIEVED ON FEBRUARY 13, 1977.  THE EMISSION
CONTROL SYSTEM FOR THIS UNIT CONSISTS OF A COLD-SIDE ESP FOLLOWED BY
TWO TCA LIME SCRUBBING MODULES SUPPLIED BY UOP. ORAVO is SUPPLYING  THE
THIOSORBIC LIME SCRUBBING REAGENT. IUCS IS SUPPLYING THEIR POZ-0-TEC
SLUDGE STABILAZATION FACILITY.
 COLUMBUS  & SOUTHERN OHIO ELEC.
 CONESVILLE NO 6
   400   MW - NEW
 COAL 4.5  - 4.9 PERCENT SULFUR
 UNIVERSAL OIL PRODUCTS
 LIME SCRUBBING
 STARTUP   10/78
THE UTILITY SIGNED LONG-TERM CONTRACTS WITH DRAVO FOR THE  PURCHASE  OF
THIOSORBIC LIME AND WITH IUCS FOK A SLUDGE FIXIATION SYSTEM.  CON-
STRUCTION OF THIS UNIT COMMENCED IN 1977 AND  IS SCHEDULED  TO  BE
COMPLETED BY JANUARY 1978. SIMILAR TO CONESVILLE NO.5,  THIS MINE MOUTH
PLANT WILL BURN COAL WITH 17 PERCENT ASH CONTENT AND 4.5 TO 4.9 PERCENT
SULFUR CONTENT. AN ELECTROSTATIC PRECIPITATOR WILL BE INSTALLED UPSTREAM
THE FGD SYSTEM. THE FGD SYSTEM WILL INCLUDE TWO TCA MODULES FOR THE  RE-
MOVAL OF S02. THE A-E DESIGN FIRM IS BLACK AND VEATCH.

-------
 COMPANY
 POWER STATION
                                             TABLE 2
                                  STATUS  OF  FGD SYSTEMS AS OF
                                                                01/78
                                                         CURRENT MONTH
COLUMBUS & SOUTHERN OHIO ELEC. THIS UNIT WILL BURN HIGH SULFUR UHIO  COAL  (APPROXIMATELY  2.5  PERCENT
P03TON NO. 5                   SULFUR CONTENT). THE DESIGN OF THE EMISSION CONTROL  STRATEGY  HAS
  375  MW - NEW                NOT YET BEEN FINALIZED.
COAL 2.5 PERCENT SULFUR
NOT SELECTED
NOT SELECTED
STARTUP   0/81
COLUMBUS & SOUTHERN OHIO ELEC. THIS UNIT WILL BURN HIGH SULFUR COAL  (APPROXIMATELY  2.5  PERCENT
POSTON NO. 6
  375  MW - NEW
COAL 2.5 PERCENT SULFUR
NOT SELECTED
NOT SELECTED
STARTUP   0/83
                               SULFUR CONTENT).  THE DESIGN OF THE EMISSION CONTROL STRATEGY
                               FOR THIS UNIT  HAS NOT YET BEEN FINALIZED.
COMMONWEALTH EDISON
POWERTON NO. 51
  425  MW • RETROFIT
COAL 3.6 PERCENT SULFUR
UNIVERSAL OIL PRODUCTS
LIMESTONE SCRUBBING
STARTUP  12/79
                               UOP WAS AWARDED THE CONTRACT FOR THE INSTALLATION OF A WET LIMESTONE
                               SCRUBBING SYSTEM THAT WILL BE BACKFITTED ONTO BOILER NO. 51, ONE OF TWO
                               IDENTICAL BOILERS SUPPLYING STEAM TO AN 850-MW TURBINE-GENERATOR. THE
                               FGD SYSTEM IS DESIGNED TO TREAT FLUE GAS RESULTING FROM THE COMBUSTION
                               OF HIGH SULFUR COAL (3.b PERCENT SULFUR* 8.3 PERCENT ASH* 17.3 PERCENT
                               MOISTURE* 10,500 BTU/LB.) AND MEET S02 EMISSION STANDARDS OF 1.8 LB.
                               S02/MM BTU.  CURRENTLY, EXCAVATION, BACKFILL, AND STRUCTURAL STEEL
                               ERECTION IS  IN PROGRESS.
 DELMARVA  POWER  CO.
 DELAWARE  CITY NOS.  1   2  &  3
   180   MW -  RETROFIT
 COKE    7-6 PERCENT  SULFUR
 DAVY POWERGAS
 WELLMAN LORD
 STARTUP   1/80
                               DELMARVA'S DELAWARE CITY PLANT HAS 
-------
 COMPANY

 POWER STATION
                                            TABU 2
                                 STATUS OF FGO SYSTEMS  AS  OF
01/78
                                                        CURRENT  MONTH
GENERAL PUBLIC UTILITIES
SEWARD NO.7
  800  MW - NEW
COAL
NOT SELECTED
NOT SELECTED
STARTUP   5/8a
                              STARTUP DATE CHANGED TO  5/84 FOR  BOTH  BOILER  AND  DESULFURIZATION  SYSTEM.
                              LIME, LIMESTONE SCRUBBING,  AND  COAL  DESULFURIZATION  ARE  THE  PRIMARY  STRA-
                              TEGIES BEING CONSIDERED  FOR COMPLIANCE WITH NEW SOURCE PERFORMANCE  STAN-
                              DARDS. NO DECISION HAS BEEN MADE  YET.
GULF POWER CO.
CRIST NO. a AND NO. 5
  150  MW - RETROFIT
                              EACH UNIT IS 75 MW.   IF  SCRUBBERS  ARE  SELECTED  THEY  WILL  BE  REQUIRED  IN
                              1976. NO DECISION HAS  YET BEEN  ANNOUNCED.
NOT SELECTED
NOT SELECTED
STARTUP   0/78
 GULF POWER CO.
 CRIST  NO. 6  AND  NO.
  820  MW -  NEW

 NOT SELECTED
 NOT SELECTED
 STARTUP   0/80
                              UNIT 6  IS  330 MW.   UNIT  7  IS  500  MW.
                              NO  DECISION  HAS  YET BEEN ANNOUNCED.
                                                                      FGD  MAY  BE  REQUIRED  IN  1980.
 GULF  POWER  CO.
 LANSING  SMITH NO.  1  AND  NO.  i
   305 MW - RETROFIT
 COAL
 NOT SELECTED
 NOT SELECTED
 STARTUP   0/80
                               UNIT  NO.  1  IS  125  MW.   UNIT  NO.  2  IS  180  MW.   IF  SCRUBBERS  ARE  SELECTED,
                               THEY  WILL BE REQUIRED  IN  1979  AND  1980  ON THE  RESPECTIVE  UNITS.
 HOOSIER  COOPERATIVE
 MEROM NO.  1
   490 MW  »  NEW
 COAL  3.5 PERCENT  SULFUR
 NOT SELECTED
 LIMESTONE  SCRUBBING
 STARTUP    0/60
                               MEROM  1  AND  2  ARE  HOOSIER  COUP'S  NEW  190  MW  COAL-FIRED  UMTS  PLANNED  FOR
                               LOCATION  IN  SULLIVAN,  INDIANA.  THE  FLUE GAS  STREAMS  WILL  BE CLEANED OF
                               PARTICULATES WITH  ESPS  (99.4X)  AND  OF  SULFUR DIOXIDE  WITH LIMESTONE
                               SCRUBBERS  C90X). SLUDGE  WILL  BE STABILIZED  AND  STOCK  PILED. THE  UTILITY
                               IS  CURRENTLY REQUESTING/EVALUATING  BIDS FOR  THE  FGD  SYSTEMS.  FGD STAKT-UP
                               DATES  ARE  SCHEDULED  FOR  LATE  1980  (NO.l)  AND MID 1981  IN0.2).
 HOOSIER  COOPERATIVE
 MEROM NO.  2
   490  MW  - NEW
 COAL 3.5 PERCENT  SULFUR
 NOT SELECTED
 LIMESTONE  SCRUBBING
 STARTUP    0/81
                               MEROM  1  AND  2  ARE  HOOSIER  COOP'S  NEW  490  MW  COAL-FIRED  UNITS  PLANNED  FUR
                               LOCATION IN  SULLIVAN,  INDIANA.  THE  FLUE GAS  STREAMS  WILL  BE  CLEANED OF
                               PARTICULATES WITH  ESPS  (99.4X)  AND  OF  SULFUR DIOXIDE WITH LIMESTONE
                               SCRUBBERS  (90X).  SLUDGE  WILL  BE STABILIZED  AND  STOCK PILED.  THE  UTILITY
                               IS  CURRENTLY REQUESTING/EVALUATING  BIDS FOR  THE FGD  SYSTEMS.  FGD START-UP
                               DATES  ARE  SCHEDULED  FOR  LATE  1980 CNO.l)  AND MID 1981  IN0.2).
 INDIANAPOLIS POWER &  LIGHT  CO.  INDIANAPOLIS  P  &  L  HAS  AWARDED  A  CONTRACT  TO UNIVERSAL OIL PRODUCTS FOR A
 PETERSBURG NO 3
   530  MW - NEW
 COAL  3.0-3.5 PERCENT SULFUR
 UNIVERSAL OIL PRODUCTS
 LIMESTONE SCRUBBING
 STARTUP  10/77
                               WET  LIMESTONE  SCRUBBING  S02  CONTROL  SYSTEM.   AN  ESP  PROVIDES PRIMARY PAR-
                               TICULATE  CONTROL.   THE  UNIT  FIRES  BITUMINOUS  COAL WITH A  SULFUR CONTENT
                               OF  3.0-3.5X,  AN  ASH CONTENT  OF  9-10X,  AND  A  HEAT CONTENT  OF  11,000
                               BTU/LB.   THE  FOUR  MODULES  OPERATED FOR 24  HOURS  IN MID-DECEMBER FOR
                               EQUIPMENT  TESTING.   THE  SCRUBBERS  WERE TAKEN  OUT OF  SERVICE  SO THAT SOME
                               FINAL  ADJUSTMENTS  COULD  BE MADE.   SCRUBBERS  ARE  EXPECTED  TO  BE BACK IN
                               SERVICE BY EARLY MARCH  1976.
INDIANAPOLIS POWER  &  LIGHT  CO.  INDIANAPOLIS  POWER  & LIGHT ANNOUNCED THAT  A  NEW  COAL-FIRED POWER
 PETERSBURG NO 4
   530  MW - NEW
 COAL 3,5 PERCENT  SULFUR
 NOT SELECTED
 LIMESTONE SCRUBBING
 STARTUP   4/82
                               GENERATING  UNIT  IS  BEING  PLANNED  FOR  THEIR PETERSBURG GENERATING STATIUN
                               LOCATED  IN  PETERSBURG,  INDIANA.  THIS  NEW UNIT  WILL FIRE HIGH-SULFUH
                               SUBBITUMINOUS  COAL  WITH A HEATING VALUE OF 11,000 BTU/LB AND ASH AND
                               SULFUR CONTENTS  OF  10  PERCENT  AND 3.5 PERCENT,  RESPECTIVELY. THE UTILITY
                               IS  NOW CONSIDERING  VARIOUS FGD STRATEGIES FOR  THE CONTROL OF SULFUR
                               DIOXIDE,  GIVING  PRIMARY CONSIDERATION TO WET LIMESTONE SCRUBBING.
                               BIOS  FOR  FGD SYSTEM ARE NOW BEING EVALUATED.

-------
 COMPANY

 POWER STATION
              TABLE 2
   STATUS OF FGD SYSTEMS AS OF
                                 01/78
                                                         CURRENT MONTH
KANSAS CITY POWER & LIGHT
HAWTHORN NO. 3
  140  MW - RETROFIT
COAL   0.5-3.5 PERCENT SULFUR
COMBUSTION ENGINEERING
LIME SCRUBBING
STARTUP  11/72
REFER TO THE BACKGROUND INFORMATION SECTION IN TABLE 3 OF THIS REPORT.
THE SCRUBBER PLANT HAS BEEN CONVERTED FROM A LIMESTONE FURNACE INJECTION
AND TAIL-END SCRUBBING SYSTEM TO A TAIL-END WET LIME SCRUBBING SYSTEM.
LIME-BASED OPERATIONS COMMENCED ON FEBRUARY 7, 1977. COMPLIANCE TESTING
FOR KANSAS CITY PARTICULATE STANDARDS INDICATED THE NO.3 UNIT WAS WELL
WITHIN THE 0.17 POUND REGULATION. THE 2-MODULE SCRUBBER PLANT CAN ONLY BE
BY-PASSEO DURING EMERGENCIES.
KANSAS CITY POWER & LIGHT
HAWTHORN NO. 4
  100  MW - RETROFIT
COAL   0.5-3.5 PERCENT SULFUR
COMBUSTION ENGINEERING
LIME SCRUBBING
STARTUP   8/72
REFER TO THE BACKGROUND INFORMATION SECTION IN TABLE 3 OF THIS REPORT.
THE SCRUBBER PLANT HAS BEEN CONVERTED FROM A LIMESTONE FURNACE INJECTION
AND TAIL-END SCRUBBING SYSTEM TO A TAIL-END WET LIME SCRUBBING SYSTEM.
OPERATIONS IN THE LIME SCRUBBING MODE COMMENCED ON JANUARY 1, 1977.
COMPLIANCE TESTING FOR KANSAS CITY PARTICULATE REGULATIONS INDICATED THE
UNIT IS MEETING THE 0.17 POUND REGULATION. THE 2-MODULE SCRUBBER PLANT
CAN ONLY BE BY-PASSED DURING EMERGENCIES.
KANSAS CITY POWER * LIGHT
LA CYGNE NO 1
  830  MW - NEW
COAL 5.0 PERCENT SULFUR
BABCOCK & WILCOX
LIMESTONE SCRUBBING
STARTUP   3/73
KANSAS POWER & LIGHT
JEFFERY NO. 1
  680  MW - NEW
COAL 0.30 PERCENT SULFUR
COMBUSTION ENGINEERING
LIMESTONE SCRUBBING
STARTUP   6/78
KANSAS POWER & LIGHT
JEFFERY NO. 2
  680  MW - NEW
COAL 0.30 PERCENT SULFUR
COMBUSTION ENGINEERING
LIMESTONE SCRUBBING
STARTUP   6/80
KANSAS POWER & LIGHT
LAWRENCE NO 4
   125  MW - RETROFIT
COAL 0.5 PERCENT SULFUR
COMBUSTION ENGINEERING
LIMESTONE SCRUBBING
STARTUP  12/68
REFER TO THE BACKGROUND INFORMATION SECTION IN TABLE 3 OF THIS REPORT.
THE EMISSION CONTROL SYSTEM FOR THIS N£« COAL-FIRED POWER-GENERATING UNIT
CONSISTS OF EIGHT SCRUBBER MODULES FOR FLY ASH AND S02 REMOVAL. EACH
MODULE INCLUDES A VENTURI SCRUBBER IN SERIES WITH A 2-STAGE IMPINGEMENT
PLATE ABSORBER.  THE SCRUBBER PLANT IS AN INTEGRAL PART OF THE POWER-
GENERATING COMPLEX, ALLOWING NO FLUE GAS BYPASS.  INITIAL OPERATIONS
COMMENCED IN FEB. 1973. COMMERCIAL SERVICE WAS ATTAINED BY JUNE 1973.
TOTAL SYSTEM AVAILABILITY FOR THE MONTH OF JANUARY WAS 94 PERCENT.

KP&L HAS PURCHASED A COMBUSTION ENGINEERING AIR QUALITY CONTROL SYSTEM
FOR PARTICULATE AND S02 REMOVAL CONSISTING OF A COLD-SIDE ESP, I.D. FANS,
BY-PASS CAPABILITY, AND SPRAY TOWERS. AN OVERFIRE AIR SYSTEM AT THE TAN-
GENTIAL FIKED PULVERIZED BURNERS WILL CONTROL NOX EMISSIONS. THE CLEANED
GASES WILL BE VENTED TO A 600 FT STACK. CONSTRUCTION IS PROCEEDING ACCORD-
ING TO SCHtDULE. THE ESP'S HAVE BEEN INSTALLED. THE SLURRY HOLD TANKS AND
ABSORBERS ARE IN PLACE. SLUDGE DISPOSAL STRATEGY HAS NOT BEEN FINALIZED.
THIS UNIT WILL FIRE 0.3X SULFUR C6X ASH) WYOMING COAL.

KP&L HAS PURCHASED A COMBUSTION ENGINEERING AIR QUALITY CONTROL SYSTEM
FOR PARTICULATE AND S02 REMOVAL CONSISTING OF A COLD-SIDE ESP, I.D. FANS,
BY-PASS CAPABILITY, AND SPRAY TOwERS. AN OVERFIHE AIM SYSTEM AT THE TAN-
GENTIAL FIRED PULVERIZED BURNERS WILL CONTROL NOX EMISSIONS. THE CLEANED
GASES WILL BE VENTED TO A 600 FT STACK. CONSTRUCTION IS PROCEEDING ACCORD-
ING TO SCHEDULE. THE ESP'S ARE NOW GOING IN. THE SLURRY HOLD TANKS AND
ABSORBERS ARE IN PLACE. SLUDGE DISPOSAL STRATEGY HAS NOT BEEN FINALIZED.
THIS UNIT WILL FIRE 0.3X SULFUR (6X ASH) WYOMING COAL.

REFER TO BACKGROUND INFORMATION SECTION IN TABLE 3 OF THIS REPORT.
THE NEW LIMESTONE FGl) SYSTEM COMMENCED OPERATIONS IN EAHLY JANUARY 1977.
THERE HAVE BEEN NO FORCED SCRUBBER OUTAGES REPORTED SINCE START-UP.
CONTINUOUS S02 MONITORS HAVE RECORDED 302 REMOVAL EFFICIENCIES OF BETTER
THAN 85X. PARTICULATE REMOVAL IS REPORTED TO BE EXCELLENT, YIELDING NO
VISIBLE PLUME.  THE PLANT IS FIRING COAL RATED AT 12,300 BTU/LB WITH A
SULFUR CONTENT OF 3.5X.
KANSAS POWER & LIGHT
LAWRENCE NO 5
  400  MW - NEW
COAL 0.5 PERCENT SULFUR
COMBUSTION ENGINEERING
LIMESTONE SCRUBBING
STARTUP  11/71
REFER TO THE BACKGROUND INFORMATION SECTION IN TABLE 3 OF THIS REPORT.
THE ORIGINAL LIMESTONE INJECTION AND TAIL-END SCRUBBING SYSTEM IS STILL
IN SERVICE WHILE A NEW ROD-SCRUBBER AND SPHAY TOWER ABSORBER SYSTEM IS
BEING ERECTED ALONG SIDE THE EXISTING SYSTEM. THE NEW SCRUBBER PLANT
INCLUDES 2 MODULES EACH CAPABLE OF HANDLING APPROXIMATELY so* OF THE TO-
TAL BOILER FLUE GAS FLOW. THE SYSTEM DESIGNER AND SUPPLIER IS COMBUSTION
ENGINEERING. THE UNIT FIRES APPROXIMATELY 140 TONS/HOUR OF LOW SULFUR
WYOMING COAL HAVING HEAT AND SULFUR CONTENTS OF 10,000 BTU/LB AND 0.5X.
KENTUCKY UTILITIES
GREEN RIVER NOS. 1  2  AND
   64  MW - RETROFIT
COAL  3.8 PERCENT SULFUR
AMERICAN AIR FILTER
LIME SCRUBBING
STARTUP   9/75
REFER TO BACKGROUND INFORMATION SECTION IN TABLE 3 OF THIS REPORT.
THE SCRUBBER PLANT INSTALLED AT THIS STATION CONSISTS OF OME MODULE
DESIGNED TO REMOVE PARTICULATES (VARIABLE-THROAT VENTURI) AND S02  (MUBILb
-BED ABSORBER) FROM COAL-FIRED BOILER FLUE GAS. THfc SCRUBBER WAS DESIGNED
AND SUPPLIED BY AAF. INITIAL SCRUBBER PLANT STARTUP OCCURRED IN SEPTEMBER
1975. SCRUBBING OPERATIONS RESUMED IN NOVEMBER FOLLOWING A 5-MONTH SHUT-
DOWN RESULTING FROM A STRIKE BY PLANT OPERATING PERSONNEL.  THE SYSTEM
HAS HAD LOW AVAILABILITY BECAUSE OF FROZEN EQUIPMENT.
                                                  10

-------
 COMPANY
 POWER STATION
                                             TABLE  2
                                  STATUS  OF  FGD  SYSTEMS AS OF
                                                                 01/78
                                                          CURRENT  MONTH
LAKELAND UTILITIES
MCINTOSH POWER PLANT UNIT NO.3
  350  MW - NEW
COAL 2.6 PERCENT SULFUR
NOT SELECTED
LIMESTONE SCRUBBING
STARTUP  10/81
                               THE  CITY  OF  LAKELAND DEPARTMENT OF ELECTRIC AND WATER UTILITIES IS EVALU-
                               ATING  BIDS  FOR  IT  NEW 350 MW POWER GENERATING UNIT, MCINTOSH NO.   3. THE
                               UNIT WILL UTILIZE  COLD-SIDE ESP'S FOR PARTICULATE REMOVAL AND LIMESTONE
                               SCRUBBING FOR  S02  CONTROL.  A DECISION SHOULD BE MADE PUBLIC IN MARCH.
                               START-UP  IS  SCHEDULED FOR OCTOBER 1981.
LOUISVILLE GAS & ELECTRIC
CANE RUN NO 4
  176  MW - RETROFIT
COAL 3.5 - 4.0 PERCENT SULFUR
AMERICAN AIR FILTER
LIME SCRUBBING
STARTUP   8/76
                               REFER  TO  THE  BACKGROUND INFORMATION SECTION IN TABLE 3 OF THIS REPORT.
                               THE  FGD  SYSTEM RETROFITTED ON THIS BOILER WAS DESIGNED AND SUPPLIED BY
                               AMERICAN  AIR  FILTER AND WAS FIRST PLACED IN THE GAS PATH ON AUGUST 7,
                               1976.   THE SYSTEM CONSISTS OF TWO PARALLEL MODULES WHICH INCLUDE MOBILE
                               BED  CONTACTORS AND OPERATE WITH A CARBIDE LIME ADDITIVE.  FOLLOWING A
                               NUMBER OF MAJOR SYSTEM MODIFICATIONS (CHEVRON-TYPE MIST ELIMINATOR, OIL
                               FIRED  REHEAT,  PLASITE DUCT LINER, HIGHER L/G), THE SYSTEM SUCCESSFULLY
                               PASSED COMPLIANCE TESTING (85X S02 REMOVAL) ON AUGUST 3 AND 4, 1977.
LOUISVILLE GAS  &  ELECTRIC
CANE RUN NO  5
   183   MW -  RETROFIT
COAL 3.5 - 4.0  PERCENT  SULFUR
COMBUSTION ENGINEERING
LIME SCRUBBING
STARTUP  4/78
 LOUISVILLE  GAS  &  ELECTRIC
 CANE  RUN  NO 6
   277   MW - RETROFIT
 COAL  3.5  -  4.0  PERCENT  SULFUR
 AOL/COMBUSTION  EQUIP  ASSOCIATE
 DOUBLE  ALKALI SCRUBBING
 STARTUP  11/79
 LOUISVILLE  GAS  &  ELECTRIC
 MILL CREEK  NO  1
   330  MW  - RETROFIT
 COAL   3.5- 4.0  PERCENT  SULFUR
 NOT  SELECTED
 LIME SCRUBBING
 STARTUP   1/82
                               COMBUSTION ENGINEERING HAS BEEN AWARDED A CONTRACT BY LG&E TO DESIGN AND
                               SUPPLY  TWO SPRAY  TOWER ABSORBERS FOR FULL-LOAD S02 REMOVAL SERVICE. THE
                               ABSORBERS WILL UTILIZE CARBIDE LIME AS THE SCRUBBING REAGENT.  IN-LINE
                               STEAM REHEAT,  A COMMON REACTION TANK,  AND A THICKENER FOR SOLIDS DEWATER-
                               ING ARE INCLUDED  IN THE FGD PLANT.   AN EXISTING UPSTREAM ESP PROVIDES
                               PRIMARY PARTICULATE CONTROL.  SYSTEM CONSTRUCTION IS NEARING COMPLETION.
                               THE START-UP DATE FOR THE SCRUBBER  PLANT HAS BEEN DELAYED UNTIL SPRING
                               BECAUSE OF THE COAL STRIKE.
                               THE CONTRACT FOR THIS FULL-SCALE DEMONSTRATION SCRUBBING SYSTEM HAS BEEN
                               AWARDED TO A .0 .LI TTLE/COMBUSTION EQUIPMENT ASSOC. FOR THE INSTALLATION
                               OF  A DOUBLE ALKALI  SCRUBBER.  THE FEDERAL EPA WILI, SUBSIDIZE A MAXIMUM
                               $4.5 MM FOR OPERATION,  RESEARCH AND DEVELOPMENT,  AND REPORT WRITING FOR
                               A ONE-YEAR PERIOD FOLLOWING THE FIRST THREE MONTHS OF OPERAT ION(NOTE*TH IS
                               SUBSIDY KILL NOT BE APPLIED FOR ANY CAPITAL EXPENDITURES). ENGINEERING
                               DESIGN WORK IS UNDERWAY. SITE PREPARATION, EXCAVATION AND FOUNDATION WORK
                               COMMENCED IN JULY.  DUCTWORK TIE-IN IS COMPLETE.

                               A COMPLIANCE SCHEDULE HAS BEEN SUBMITTED TO THE JEFFERSON COUNTY AIR POL-
                               LUTION CONTROL DISTRICT WITH  1/82 ESTABLISHED AS  THE STARTUP DATE FOR AN
                               FGD SYSTEM. OPERATING DATA AND INFORMATION FROM THE FULL-SCALE SCRUBBER
                               PLANT NOW IN SERVICE ON THE NO.4 UNIT AT CANE HUN WILL BE OBTAINED BEFORE
                               THE UTILITY PROCEEDS WITH ADDITIONAL SYSTEM DESIGN WORK.
 LOUISVILLE  GAS &  ELECTRIC       A  COMPLIANCE  SCHEDULE  HAS  BEEN  SUBMITTED  TO THE  JEFFERSON COUNTY  AIR POL-
 MILL CREEK  NO 2                LUTION  CONTROL  DISTRICT  WITH  1/81  ESTABLISHED  AS THE  STARTUP DATE FOR AN
   330  MW - RETROFIT            FGD  SYSTEM. OPERATING  DATA AND  INFORMATION  FROM  THE  FULL-SCALE SCRUBBER
 COAL   3.5- 4.0 PERCENT  SULFUR  PLANT NOW  IN  SERVICE ON  THE NO.4  UNIT  AT  CANE  RUN WILL BE OBTAINED BEFORE
 NOT SELECTED                   THE  UTILITY PROCEEDS WITH  ADDITIONAL  SYSTEM DESIGN WORK.
 LIME SCRUBBING
 STARTUP   1/81
 LOUISVILLE GAS &  ELECTRIC
                               BECAUSE POWER DEMAND HAS NOT COME UP AS RAPIDLY AS HAD BEEN EXPECTED,
 MILL CREEK  NO 3                UNIT  START-UP  HAS  BEEN  MOVED  BACK  TO  APRIL  15,  1976.  CONSTRUCTION ON
   425  MW - NEW                THIS  NEW  FACILITY'S  FGD SYSTEM  IS  NEARING  COMPLETION. THE SYSTEM IS DE-
 COAL   3.5- 4.0 PERCENT  SULFUR  SIGNED  AND  SUPPLIED  BY  AMERICAN AIR FILTER  AND  WILL UTILIZE CARBIDE LIME
                                AS  THE  ABSORBENT.  FOUR  MOBILE-BED  ABSORBERS WILL  TREAT THE FLUE GAS RE-
                                SULTING FROM THE COMBUSTION OF  HIGH SULFUR  COAL.  THE  SYSTEM WILL OPERATE
                                IN  A  CLOSED WATER  LOOP. THE SCRUBBING WASTE WILL  BE STABILIZED WITH
                                FLYASH  AND  LIME.
AMERICAN AIR FILTER
LIME SCRUBBING
STARTUP   4/78
 LOUISVILLE GAS & ELECTRIC       BECAUSE  POWER  DEMAND  HAS  NOT  COME  UP AS RAPIDLY AS HAD BEEN EXPECTED,
 MILL CREEK NO 4                UNIT  START-UP  HAS  BEEN  MOVED  BACK  TO JUNE  1980.  CONSTRUCTION OF THIS NEW
   495  MW - NEW                495-MW COAL-FIRED  UNIT  IS ON  SCHEDULE.   CURRENTLY, FOUNDATION WORK IS IN
 COAL   3.5- 4.0 PERCENT  SULFUR  PROGRESS.   THIS  AAF  SYSTEM WILL  INCLUDE MOBILE-BED ABSORBERS TREATING
 AMERICAN AIR FILTER             HIGH  SULFUR COAL FLUE GAS.  THE  SYSTEMS WATER LOOP WILL BE CLOSED.  THE
 LIME SCRUBBING                 SLUDGE WILL BE STABILIZED WITH LIME  AND FLYASH.  STEAM REHEAT WILL PRO-
 STARTUP   6/80                 VIDE  GAS TEMPERATURE  ELEVATION OF  THE SCRUBBED GASES PRIOR TO DISCHARGE
                                TO  THE MAIN STACK.
                                                   11

-------
 COMPANY
 POWER STATION
                                             TABLE 2
                                  STATUS OF FGD SYSTEMS AS OF
                                                                01/78
                                                         CURRENT MONTH
LOUISVILLE GAS & ELECTRIC
PADDYS RUN NO 6
   65  MW - RETROFIT
COAL 3.5 - 4.0 PERCENT SULFUR
COMBUSTION ENGINEERING
LIME SCRUBBING
STARTUP   4/73
                               REFER TO THE BACKGROUND INFORMATION SECTION IN TABLE 3 OF THIS  REPORT.
                               THIS SCRUBBING SYSTEM WAS DESIGNED BY COMBUSTION ENGINEERING AND  PLACED
                               IN SERVICE IN APRIL 1973.  THE FGO SYSTEM CONSISTS OF TWO 2-STAGE  MARBLE
                               BED ABSORBERS WHICH ARE DESIGNED TO USE CARBIDE LIME ADDITIVE AS  THE
                               SCRUBBING REAGENT.  PADDYS RUN NO.  IS A PEAK-LOAD UNIT THAT OPERATES
                               ONLY DURING DEMAND PERIODS.  AN EXTENSIVE EPA SCRUBBER/SLUDGE EVALUATION
                               STUDY WAS COMPLETED IN AUGUST 1977.
                               MINNESOTA P S L HAS AWARDED A CONTRACT TO PEABODY ENGINEERING  FOR  A  LIME/
                               ALKALINE FLYASH S02 CONTROL SYSTEM. THE CONFIGURATION WILL  BE  VENTUHI
                               SCRUBBERS FOLLOWED BY SPRAY TOWERS. HOT SIDE ESP'S WILL BE  USED  FOR
                               PARTICULATE CONTROL. STACK GAS REHEAT WILL 6E ACCOMPLISHED  BY  BYPASSING
                               5X OF FLUE GAS AROUND THE SCRUBBER. THE UNIT WILL FIRE SUB-BITUMINOUS
LIME/ALKALINE FLYASH SCRUBBING COLSTR1P COAL WITH A SULFUR CONTENT OF 0.8X, AND AN  ASH CONTENT  OF  9.OX
STARTUP   0/80                 CHEATING VALUE - 8300 BTU/LB). MAKE-UP WATER SOURCE  WILL  BE THE  RIVER  OR
                               THE CLAY-LINED POND.
MINNESOTA POWER AND LIGHT co.
CLAY BOSWELL NO. 4
  500  MW - NEW
COAL 0.8 PERCENT SULFUR
PEABODY ENGINEERING
MINNKOTA POWER COOPERATIVE
MILTON R. YOUNG NO. 2
  450  MW - NEW
LIGNITE 0.7 PERCENT SULFUR
AOL/COMBUSTION EQUIP ASSOCIATE
LIME/ALKALINE FLYASH SCRUBBING
STARTUP   9/77
MONTANA POWER CO.
COLSTRIP NO  1
  360  MW -  NEW
COAL 0.8 PERCENT SULFUR
AOL/COMBUSTION EQUIP ASSOCIATE
LIME/ALKALINE FLYASH SCRUBBING
STARTUP  11/75
MONTANA POWER CO.
COLSTRIP NO 2
  360  MW - NEW
COAL 0.8 PERCENT SULFUR
AOL/COMBUSTION EQUIP ASSOCIATE
LIME/ALKALINE FLYASH SCRUBBING
STARTUP   7/76
MONTANA  POWER CO.
COLSTRIP NO. 3
  700  MW - NEW
COAL   0.7 PERCENT SULFUR
ADL/COMBUSTION EQUIP ASSOCIATE
LIME/ALKALINE FLYASH SCRUBBING
STARTUP   7/80
                               REFER TO THE BACKGROUND INFORMATION SECTION IN TABLE 3 OF THIS REPORT.
                               THIS LIME/ALKALINE FLYASH SCRUBBING SYSTEM WAS DESIGNED AND SUPPLIED BY
                               AOL/CONTRUCTION EQUIPMENT ASSOCIATEES. IT CONSISTS OF A COLD-SIDE ESP
                               FOLLOWED BY TWO SPRAY TOWERS.  MIST ELIMINATION IS PROVIDED BY A WASH
                               TRAY AND CHEVRON ARRANGEMENT.  25* FLUE GAS BYPASS PROVIDES STACK GAS RE-
                               HEAT.  THE UNIT FIRES A LOW-SULFUR NORTH DAKOTA LIGNITE WITH AN AVERAGE
                               ASH CONTENT OF 8 PERCENT, SULFUR CONTENT OF 0.7 PERCENT, AND HEAT CONTENT
                               OF 6500 BTU/LB.

                               REFER TO THE BACKGROUND INFORMATION SECTION IN TABLE 3 OF THIS REPORT.
                               THIS FGD EQUIPPED UNIT WAS DECLARED COMMERCIAL IN NOVEMBER 1975.  THE
                               SCRUBBING SYSTEM PROVIDES PARTICULATE AND S02 CONTROL WITH THREE SCRUB-
                               BER MODULES.  EACH MODULE CONSISTS OF A OOWNFLOW VENTURI SCRUBBER CENTER-
                               ED WITHIN AN UPFLOW SPRAY TOWER ABSORBER.  EACH MODULE CAN TREAT 40X OF
                               THE TOTAL BOILER FLUE GAS AND THE MODULES CANNOT BE BYPASSED.  THE UN-
                               STABILIZED SLUDGE IS DISPOSED IN AN ON-SITE LINED DISPOSAL POND.  IN-LINE
                               STEAM REHEAT AND CLOSED WATER LOOP CAPABILITY ARE INCLUDED IN THE SYSTEM.

                               REFER TO THE BACKGROUND INFORMATION SECTION IN TABLE 3 OF THIS REPORT.
                               THIS FGD EQUIPPED UNIT WAS DECLARED COMMERCIAL IN AUGUST 1976.  THE
                               SCRUBBING SYSTEM PROVIDES PARTICULATE AND S02 CONTROL WITH THREE SCRUB-
                               BER MODULES.  EACH .MODULE CONSISTS OF A DOWNFLOW VENTURI SCRUBBER CENTER-
                               ED WITHIN AN UPFLOW SPRAY TOWER ABSORBER.  EACH MODULE CAN TREAT 70X OF
                               THE TOTAL BOILER FLUE GAS AND THt MODULES CANNOT BE BYPASSED.  THE UN-
                               STABILIZED SLUDGE IS DISPOSED IN AN ON-SITE LINED DISPOSAL POND.  IN-LINE
                               STEAM REHEAT AND CLOSED WATER LOOP CAPABILITY ARE INCLUDED IN THE SYSTEM.

                               A CONTRACT FOR THE INSTALLATION OF TWO ADDITIONAL LIME/ALKALINE FLYASH
                               SCRUBBING SYSTEMS HAS BEEN AWARDED TO A.D. LITTLE/COMBUSTION EQUIPMENT
                               ASSOCIATES. THESE SYSTEMS WILL BE INSTALLED ON UNITS NOS. 3 AND 4 OF
                               THE COLSTRIP POWER STATION. COLSTRIP UNITS 1 AND 2 ARE BOTH EQUIPPED
                               WITH OPERATIONAL LIME/ALKALINE FLYASH SCRUBBING SYSTEMS FOR THE REMOVAL
                               OF PARTICULATES AND SULFUR DIOXIDE. ENGINEERING WORK FOR THE NEW SYSTEMS
                               IS NOW UNDERWAY. THIS CONTRACT IS EXPECTED TO EXCEED S50 MM.
MONTANA POWER CO.
COLSTRIP NO. 4
  700  MW - NEW
COAL  0.7 PERCENT SULFUR
                               A CONTRACT FOR THE INSTALLATION OF TWO ADDITIONAL LIME/ALKALINE FLYASH
                               SCRUBBING SYSTEMS HAS BEEN AWARDED TO A.D. LITTLE/COMBUSTION EQUIPMENT
                               ASSOCIATES. THESE SYSTEMS WILL BE INSTALLED ON UNITS NOS. 3 AND 4 OF
                               THE COLSTRIP POWER STATION. COLSTRIP UNITS 1 AND 2 ARE BOTH EQUIPPED
 ADL/COMBUSTION EQUIP ASSOCIATE WITH OPERATIONAL LIME/ALKALINE FLYASH SCRUBBING SYSTEMS FOR  THE  REMOVAL
 LIME/ALKALINE FLYASH SCRUBBING OF PARTICULATES AND SULFUR DIOXIDE. ENGINEERING WORK FOR  THE  NEW SYSTEMS
 STARTUP   7/81                 IS NOW UNDERWAY. THIS CONTRACT IS EXPECTED TO EXCEED $50  MM.
NEVADA POWER
HARRY ALLEN STATION NO.
  500  MW - NEW
COAL
NOT SELECTED
NOT SELECTED
STARTUP   6/83
                               CONSIDERING HOT SIDE ESP IN CONJUNCTION WITH AN FGD SYSTEM.
                               TIONS HAVE NOT YET BEEN PREPARED.
SPECIFICA-
                                                  12

-------
 COMPANY

 POWER STATION
              TABLE 2
   STATUS OF F6D SYSTEMS AS OF
       01/78

CURRENT MONTH
NEVADA POWER
HARRY ALLEN STATION NO. 2
  500  MW - NEW
COAL
NOT SELECTED
NOT SELECTED
STARTUP   6/84
CONSIDERING HOT SIDE ESP IN CONJUNCTION WITH AN FGD SYSTEM.  SPECIFICA-
TIONS HAVE NOT YET BEEN PREPARED.
NEVADA POWER
HARRY ALLEN STATION NO.
  500  MW • NEW
COAL
NOT SELECTED
NOT SELECTED
STARTUP   6/85
CONSIDERING HOT SIDE ESP IN CONJUNCTION WITH AN FGD SYSTEM.
TIONS HAVE NOT YET BEEN PREPARED.
                                   SPECIFICA-
NEVADA POWER
HARRY ALLEN STATION NO.
  500  MW - NEW
COAL
NOT SELECTED
NOT SELECTED
STARTUP   6/66
CONSIDERING HOT SIDE ESP IN CONJUNCTION WITH AN FGO SYSTEM.
TIONS HAVE NOT YET BEEN PREPARED.
                                                                                             SPECIFICA-
 NEVADA  POWER
 REID  GARDNER  NO  1
   125  MW  - RETROFIT
 COAL  0.5 -  1.0 PERCENT  SULFUR
 AOL/COMBUSTION EQUIP  ASSOCIATE
 SODIUM  CARBONATE SCRUBBING
 STARTUP   4/74
 NEVADA  POWER
 REID  GARDNER  NO  2
   125  MW  - RETROFIT
 COAL  0,5 - 1.0 PERCENT  SULFUR
 ADL/COMBUSTION EQUIP  ASSOCIATE
 SODIUM  CARBONATE SCRUBBING
 STARTUP   4/74
 NEVADA  POWER
 REID  GARDNER  NO 3
   125  MW  - NEW
 COAL  0.5  - 1.0  PERCENT  SULFUR
 ADL/COMBUSTION  EQUIP  ASSOCIATE
 SODIUM  CARBONATE SCRUBBING
 STARTUP   7/76
 NEVADA  POWER
 REID  GARDNER  NO 4
   125  MW  -  NEW
 COAL    0-5-  1.0 PERCENT  SULFUR
 AOL/COMBUSTION  EQUIP  ASSOCIATE
 SODIUM  CARBONATE SCRUBBING
 STARTUP   O/  0
REFER TO THE BACKGROUND INFORMATION SECTION IN TABLE 3 (JF THIS REPORT.
THIS SODIUM CARBONATE-BASED (TRONA) SCRUBBING SYSTEM CONSISTS OF ONE
MODULE CONTAINING A TWIN VARIABLE-THROAT VENTURI SCRUBBER FOLLOWED BY  A
SEPARATOR IN SERIES WITH A SINGLE-STAGE PERFORATED-PLATE ABSORBER TOWER.
PRIMARY. PARTICULATE CONTROL IS PROVIDED BY UPSTREAM MECHANICAL COLLECTORS.
A STEAM INDIRECT HOT AIR REHEAT SYSTEM RAISES THE GAS TEMPERATURE 30 F
PRIOR TO DISCHARGE TO THE MAIN STACK. THE FLUE GAS CLEANING WASTES ARE
ULTIMATELY DISPOSED IN AN ON-SITE CLAY-LINED SOLAR EVAPORATION POND.

REFER TO THE BACKGROUND INFORMATION SECTION IN TABLE 3 OF THIS REPORT.
THIS SODIUM CARBONATE-BASED (TRONA) SCRUBBING SYSTEM CONSISTS OF ONE
MODULE CONTAINING A TWIN VARIABLE-THROAT VENTURI SCRUBBER FOLLOWED BY  A
SEPARATOR IN SERIES WITH A SINGLE-STAGE PERFORATED-PLATE A8SOR8ER TOWER.
PRIMARY PARTICULATE CONTROL IS PROVIDED BY UPSTREAM MECHANICAL COLLECTORS.
A STEAM INDIRECT HOT AIR REHEAT SYSTEM RAISES THE GAS TEMPERATURE 30 F
PRIOR TO DISCHARGE TO THE MAIN STACK. THE FLUE GAS CLEANING WASTES ARE
ULTIMATELY DISPOSED IN AN ON-SITE CLAY-LINED SOLAR EVAPORATION POND.

REFER TO THE BACKGROUND INFORMATION SECTION IN TABLE 3 OF THIS REPORT.
THIS UNIT IS A NEW COAL-FIRED BOILER THAT IS EQUIPPED WITH SODIUM
CARBONATE-BASED(TRONA)SCRUBBING SYSTEM WHICH INCORPORATES A TWIN
VARIABLE-THROAT VENTURI SCRUBBER FOLLOWED BY A SEPARATOR IN SERIES WITH
A SINGLE-STAGE PERFORATED-PLATE ABSORBER TOWER.  THE MODULE WAS FIRST
PLACED IN SERVICE ON BOILER FLUE GAS IN JULY 1976.  MECHANICAL COLLECTORS
PROVIDE PRIMARY PARTICULATE CONTROL.  REHEAT -IS PROVIDED BY A STEAM  IN-
DIRECT HOT AIR RtHEAT SYSTEM.  WASTE DISPOSAL IS ON-SITE CLAY-LINED  POND.

NEVADA POWER COMPANY HAS SIGNED A LETTER OF INTENT WITH COMBUSTION EQUIP-
MENT ASSOCIATES FOR THE CONSTRUCTION OF AN FGO SYSTEM ON REID GARDNER  NO.
1.  HOWEVERf CONSTRUCTION OF THE BOILER HAS BEEN INDEFINITELY POSTPONED.
 NEVADA  POWER
 WARNER  VALLEY  STATION  NO.
   250   MW  - NEW
 COAL
 NOT SELECTED
 NOT SELECTED
 STARTUP   6/82
SPECIFICATIONS ARE BEING PREPARED FOR A SCRUBBING SYSTEM.  NEVADA POWER
HAS NOT YET ANNOUNCED PLANS FOR THIS UNIT'S EMISSION CONTROL STRATEGY.
                                                  13

-------
 COMPANY

 POWER STATION
              TABLE 2
   STATUS OF FGD SYSTEMS AS OF
                                 01/78

                          CURRENT MONTH
NEVADA POWER
WARNER VALLEY STATION NO. 2
  250  MW • NEW
COAL
NOT SELECTED
NOT SELECTED
STARTUP   6/83
SPECIFICATIONS ARE BEING PREPARED FOR A SCRUBBING SYSTEM.  NEVADA POWER
HAS NOT YET ANNOUNCED PLANS FOR THIS UNIT'S EMISSION CONTROL STRATEGY.
NEW ENGLAND ELEC SYSTEM
BRAYTON POINT NO.3
  650  MW - RETROFIT
COAL 3.0 PERCENT SULFUR
NOT SELECTED
REGENERABLE NOT SELECTED
STARTUP   O/ 0
THE UTILITY IS CURRENTLY INVESTIGATING VARIOUS ADVANCED REGENERABLE
FLUE GAS DESULFURIZATION SYSTEMS WHICH OFFER A BREAKTHROUGH IN
OPERATING COSTS AND PRODUCE ELEMENTAL SULFUR AS AN END
PRODUCT.  THE UTILITY IS CURRENTLY INVOLVED IN BENCH AND LABORATORY
SCALE INVESTIGATIONS OF SULFUR RECOVERY.  THE NO. 3 UNIT IS CURRENTLY
OPERATIONAL,  FIRING LOW SULFUR FUEL OIL.
NIAGARA MOHAWK POWER COOP.
CHARLES R. HUNTLEY NO.6
   100  MW - RETROFIT
COAL 2.5-4.5 PERCENT SULFUR
ATOMICS INTERNATIONAL
AOUEDUS CARBONATE SCRUBBING
STARTUP   0/80
A CONTRACT WAS AWARDED TO ATOMICS INTERNATIONAL FOR THE DESIGN AND IN-
STALLATION OF AN AQUEOUS CARBONATE FGD SYSTEM. THIS DEMONSTRATION SYSTEM
WILL PRODUCE END-PRODUCT SULFUR. FUNDS ARE BEING PROVIDED BY THE US EPA
AND THE EMPIRE STATE ELECTRIC ENERGY RESEARCH CORP. THE DESIGN S02 RE-
MOVAL EFFICIENCY WILL BE 90 PERCENT. AN INTERMEDIATE UNIT IS BEING CON-
SIDERED AS A PILOT BEFORE APPLICATION OF THE JOO MW SCALE UNIT. GROUND
BREAKING FOR CONSTRUCTION WILL BE IN JUNE 1978.
NORTHERN  INDIANA PUB SERVICE
BAILLY NO. 7
   190  MW - RETROFIT
COAL 3 PERCENT SULFUR
NOT SELECTED
NOT SELECTED
STARTUP   O/ 0
CONSIDERING A LIME OR LIMESTONE SCRUBBING UNIT.  ALSO WAITING FOR PER-
FORMANCE OF WELLMAN LORD/ALLIED CHEMICAL UNIT IN SERVICE AT THEIR
D.H, MITCHEL NO. 11 UNIT. LOW SULFUR COAL MAY BE EMPLOYED TO COMPLY WITH
S02 EMISSION REGULATIONS. APPLICABLE INDIANA S02 REGULATIONS ARE STILL
NOT FIRMLY ESTABLISHED.
NORTHERN  INDIANA PUB SERVICE
BAILLY NO. 8
  400  MW - RETROFIT
COAL 3 PERCENT SULFUR
NOT SELECTED
NOT SELECTED
STARTUP   O/ 0
CONSIDERING A LIME OR LIMESTONE SCRUBBING UNIT.  ALSO WAITING FOR PERFOR-
MANCE OF WELLMAN LORD/ALLIED CHEMICAL UNIT UNDER CONSTRUCTION AT THEIR
D. H. MITCHELL NO. 11 UNIT.  LOW SULFUR COAL MAY BE BURNED TO COMPLY WITH
S02 EMISSION REGULATIONS. APPLICABLE INDIANA S02 REGULATIONS ARE STILL
NOT FIRMLY ESTABLISHED.
NORTHERN  INDIANA PUB SERVICE
O.H. MITCHELL NO.11
   115  MW - RETROFIT
COAL 3.2-3.5 PERCENT SULFUR
DAVY POWERGAS/ALLIED CHEMICAL
WELLMAN LORD/ALLIED CHEMICAL
STARTUP   6/77
REFER TO THE BACKGROUND INFORMATION SECTION IN TABLE 3 OF THIS REPORT.
THIS FGD SYSTEM IS AN INTEGRATION OF THE WELLMAN-LORD S0£ RECOVERY PROCES
OFFERED BY DAVY POWERGAS AND THE 302 TO SULFUR REDUCTION PROCESS DE-
VELOPED BY ALLIED CHEMICAL. DAVY POWERGAS IS THE DESIGN AND CONSTRUCTION
FIRM AND ALLIED CHEMICAL IS SYSTEM OPERATOR AND PRODUCT MARKETER.
PERFORMANCE TESTS WERE SUCCESSFULLY COMPLETED ON SEPTEMBER 14, 1977. A
DEMONSTRATION YEAR COMMENCED ON SEPTEMBER 16, 1977.
NORTHERN STATES POWER CO.
SHERBURNE COUNTY STATION NO.l
  710  MW - NEW
COAL 0.8 PERCENT SULFUR
COMBUSTION ENGINEERING
LIMESTONE SCRUBBING
STARTUP   3/76
REFER TO THE BACKGROUND INFORMATION SECTION IN TABLE 5 OF THIS REPORT.
FULL COMMERCIAL OPERATION OF THE SYSTEM BEGAN ON MAY i, 1976. THE SCRUB-
BING SYSTEM FOR THIS UNIT CONSISTS OF 12 MODULES. EACH SCRUBBING MODULE
INCORPORATES A VENTURI-ROO SECTION AND A MARBLE BED ABSORBER FOR PAH-
TICULATE AND SULFUR DIOXIDE REMOVAL. A FORCED OXIDATION SYSTEM CONVERTS
ALL THE CALCIUM SULFITE TO SULFATE PRIOR TO DISCHARGE TO A CLAY-LINED
SETTLING POND. STACK GAS REHEAT IS PROVIDED BY IN-LINE HOT WATER TUBES.
NORTHERN STATES POWER CO.
SHERBURNE COUNTY STATION NO.2
  710  MW - NEW
COAL 0.8 PERCENT SULFUR
COMBUSTION ENGINEERING
LIMESTONE SCRUBBING
STARTUP   4/77
REFER TO THE BACKGROUND INFORMATION SECTION IN TABLE 3 OF THIS REPORT,
THE SHERBURNE NO. 2 AIR QUALITY CONTROL SYSTEM IS IDENTICAL IN DESIGN TO
THE SYSTEM IN OPERATION ON THE NO. 1 UNIT AT THIS STATION. TWELVE 2-STAGE
PARTICULATE SCRUBBER (VENTURI-ROD SCRUBBER) AND SULFUR DIOXIDE ABSORBER
(MARBLE-BED ABSORBER)  MODULES ARE PROVIDED FOR FLY ASH AND S02 CONTROL.
ELEVEN MODULES ARE REQUIRED FOR FULL GENERATING CAPACITY OPERATIONS.
THE CALCIUM SULFITE IS FORCIBLY OXIDIZED TO SULFATE PRIOR TO DISCHARGE TO
THE DISPOSAL POND. STACK GAS REHEAT PROVIDED BY IN-LINE HOT WATER TUBES.

-------
 COMPANY

 POWER STATION
              TABLE 2
   STATUS OF FGD SYSTEMS AS OF
       01/78

CURRENT MONTH
NORTHERN STATES POWER CO.
SHERBURNE COUNTY STATION NO.3
  860  MW - NEW
COAL 0.8 PERCENT SULFUR
COMBUSTION ENGINEERING
LIMESTONE SCRUBBING
STARTUP   5/81
NORTHERN STATES POWER CO.
SHERBURNE COUNTY STATION NO.4
  860  MW - NEW
COAL 0.8 PERCENT SULFUR
COMBUSTION ENGINEERING
LIMESTONE SCRUBBING
STARTUP   5/83
OTTER  TAIL POWER  COMPANY
COYOTE  NO. 1
   400   MW - NEW
LIGNITE 0.9 PERCENT  SULFUR
WHEELABRATOR-FRYE/A.I.
AQUEOUS CARBONATE/FAB.  FILTER
STARTUP  5/81
 PACIFIC  GAS  AND  ELECTRIC
 FOSSIL NO.  1
   800  MW  *  NEW
 COAL  0.8 PERCENT SULFUR
 NOT  SELECTED
 LIMESTONE  SCRUBBING
 STARTUP    0/84
TWO ADDITIONAL COAL-FIRED POWER-GENERATING UNITS ARE SCHEDULED TO BE IN-
STALLED AT NSP'S SHERBURNE COUNTY GENERATING STATION IN BECKER MINNESOTA.
COMBUSTION ENGINEERING WAS AWARDED A CONTRACT FOR LIMESTONE SLURRY SPRAY
TOWER FGO SYSTEMS ON THE 860 MW UNITS 344. THE TWO STAGE SCRUBBING
MODULES REMOVE PARTICULATE (99.5X) & 302  (60X). COMMERCIAL START-UP DATES
ARE NOW SCHEDULED FOR MAY 1981 AND MAY 1983. THE BOILER CONTRACT HAS BEEN
AWARDED TO BABCOCK AND WILCOX AND THE TURBINE WILL BE SUPPLIED BY GENERAL
ELECTRIC. CONSTRUCTION IS SCHEDULED TO COMMENCE DURING THE SUMMER OF '78.

TWO ADDITIONAL COAL-FIRED POWER-GENERATING UNITS ARE SCHEDULED TO BE IN-
STALLED AT NSP'S SHERBURNE COUNTY GENERATING STATION IN BECKER MINNESOTA.
COMBUSTION ENGINEERING WAS AWARDED A CONTRACT FOR LIMESTONE SLURRY SPRAY
TOWER FGD SYSTEMS ON THE 860 MW UNITS 3*4. THE TWO STAGE SCRUBBING MOD-
ULES REMOVE PARTICULATE  C99.5X) AND 302  180X). COMMERCIAL START-UP DATES
ARE NOW SCHEDULED FOR MAY 1981 AND MAY 1983. THE BOILER CONTRACT HAS BEEN
AWARDED TO BABCOCK AND WILCOX AND THE TURBINE WILL BE SUPPLIED BY GENERAL
ELECTRIC.

THIS NEW COAL-FIRED STATION IS JOINTLY OWNED BY FIVE UTILITIES. OTTER
TAIL POWER IS THE MAJOR OWNER AND CONSTRUCTOR. MONTANA-DAKOTA UTILITIES
IS THE FACILITY OPERATOR. THIS PLANNED UNIT WILL FIRE LOW SULFUR LIGNITE
FROM THE MERCER COUNTY AREA IN ITS 8&W CYCLONE-FIRED BOILER. THE CONTRACT
FOR THIS AQUEOUS CARBONATE/FABRIC FILTER  SU2 SCRUBBER WAS AWARDED TO
WHEELABRATOR-FRYE. AND ATOMICS INTERNATIONAL. THE DRY REMOVAL SYSTEM COM-
BINES THE OPEN LOOP OF AI'S AQUEOUS CARBONATE PROCESS WITH A W-F FABRIC
FILTER. ACTUAL PLANT CONSTRUCTION BEGAN  SEPT. 77. START-UP SET FOR MAY 81.

THE CITY OF LAKELAND DEPARTMENT OF ELECTRIC AND WATER UTILITIES IS EVALU-
ATING BIDS FOR IT NEW 350 MW POWER GENERATING UNIT, MCINTOSH NO.   3. THE
UNIT WILL UTILIZE COLD-SIDE ESP'S FOR PARTICULATE REMOVAL AND LIMESTONE
SCRUBBING FOR S02 CONTROL. A DECISION SHOULD BE MADE-PUBLIC IN MARCH.
START-UP IS SCHEDULED FOR OCTOBER 1981.
 PACIFIC GAS AND ELECTRIC
 FOSSIL NO.  2
   800  MW - NEW
 COAL 0.8 PERCENT SULFUR
 NOT SELECTED
 LIMESTONE SCRUBBING
 STARTUP   0/85
THE CITY OF LAKELAND DEPARTMENT OF ELECTRIC AND WATER UTILITIES  IS EVALU-
ATING BIDS FOR IT NEW 350 MW POWER GENERATING UNIT, MCINTOSH NO.   3.  THE
UNIT WILL UTILIZE COLD-SIDE ESP'S FOR PARTICULATE REMOVAL  AND LIMESTONE
SCRUBBING FOR S02 CONTROL. A DECISION SHOULD BE MADE PUBLIC IN MARCH.
START-UP IS SCHEDULED FOR OCTOBER 1981.
 PACIFIC POWER AND LIGHT CO.
 JIM BRIDGER NO. 4
   509  MW - NEW
 COAL 0.56 PERCENT SULFURCAVG.)
 UNIVERSAL OIL PRODUCTS
 SODIUM CARBONATE SCRUBBING
 STARTUP   9/79
 PENNSYLVANIA POWER CO.
 BRUCE MANSFIELD NO. 1
   825  MW - NEW
 COAL 4.7 PERCENT SULFUR
 CHEMICO
 LIME SCRUBBING
 STARTUP   4/76
 PENNSYLVANIA POWER CO.
 BRUCE MANSFIELD NO. 2
   825  MM - NEW
 COAL 4.7 PERCENT SULFUR
 CHEMICO
 LIME SCRUBBING
 STARTUP   7/77
UOP WAS AWARDED A CONTRAST FOR THE INSTALLATION OF THE FGD  SYSTEM  AT  THE
NEW 509 MW COAL-FIRED JIM BRIDGER UNIT NO. 4.  THE FGD SYSTEM  WILL  CONSIST
OF THREE PARALLEL ABSORBER MODULES  EACH TREATING ONE-THIRD OF  THE BOILER
FLUE GAS AT FULL LOAD. AN ESP WILL PROVIDE PRIMARY PARTICULATE  CONTROL.
A CEILCOTE-LINEO WET/DRY STACK IS INCLUDED IN  THE SYSTEM. PPL'S PILOT
STUDY  INSPECTION REVEALED SCALE FORMATION PROBLEMS.  TESTS ARE BEING CON-
DUCTED TO RESOLVE THIS PROBLEM. TO DATE, FOUNDATION  CONSTRUCTION  IS
COMPLETE AND VESSEL ERECTION HAS COMMENCED.

THIS EMISSION CONTROL SYSTEM WAS DESIGNED TO REMOVE  FLYASH  AND  SOS FROM
3,35 MM ACFM OF FLUE GAS VIA WET LIME SCRUBBING. THE  INITIAL  SHAKEDOWN
AND DEBUGGING PHASE OF OPERATION BEGAN FOR PART OF THE SYSTEM IN  DECEMBER
1975.  PARTIAL COMMERCIAL OPERATION COMMENCED IN APRIL 1976. THE UNIT  WAS
CERTIFIED FULL-LOAD COMMERCIAL IN JUNE 1976. THE FGD  SYSTEM HAS EXPERI-
ENCED  OPERATIONAL PROBLEMS SINCE IT HAS BEEN IN SERVICE  REQUIRING  A NUM-
BER OF SYSTEM REPAIRS AND DESIGN MODIFICATIONS. REFER TO BACKGROUND IN-
FORMATION SECTION IN TABLE 5 OF THIS REPORT FOR GREATER  DETAIL.

REFER  TO THE BACKGROUND INFORMATION SECTION IN TABLE  3 OF THIS  REPORT.
THIS EMISSION CONTROL SYSTEM WAS DESIGNED TO REMOVE  FLYASH  AND  302 FROM
3.35 MM ACFM OF FLUE GAS USING THIOSORBIC LIME AS A  SCRUBBING ABSORBENT.
SIX SCRUBBING TRAINS, EACH INCLUDING TWO VENTURI SCRUBBERS  IN SERIES
ARRANGEMENT, ARE PROVIDED FOR FULL-LOAD OPERATION.   THE  INITIAL SHAKEDOWN
AND DEBUGGING PHASE OF OPERATION BEGAN FOR THREE TRAINS  IN  JULY,  1977.
FULL COMMERCIAL OPERATION FOR THE ENTIRE SYSTEM COMMENCED ON  OCTOBER  1,
1977.
                                                  15

-------
 COMPANY

 POWER STATION
              TABLE 2
   STATUS OF FGD SYSTEMS AS OF
                                 01/78
                                                         CURRENT MONTH
PENNSYLVANIA POWEH CO.
BRUCE MANSFIELD NO. 3
  825  MM - NEW
COAL 4.7 PERCENT SULFUR
PULLMAN KELLOGG
LIME SCRUBBING
STARTUP   4/80
THE PULLMAN KELLOGG DIVISION OF PULLMAN INCORPORATED HAS BEEN AWARDED
A CONTRACT IN EXCESS OF $50 MILLION BY THE CAPCO CONSORTIUM FOR THE  IN-
STALLATION OF SULFUR DIOXIDE ABSORBERS ON THIS 825 MM COAL-FIRED POWER-
GENERATING UNIT.  THE EMISSION CONTROL SYSTEM FOR THIS UNIT WILL CONSIST
OF ESP'S UPSTREAM OF FIVE WEIR HORIZONTAL CROSSFLOW WET SCRUBBING MOD-
ULES.  CONSTRUCTION OF THE BOILER IS CURRENTLY IN PROGRESS.  DUE TO  RE-
VISED CAPCO FORECASTS, UNIT START-UP HAS BEEN MOVED BACK TO APRIL 1980.
PHILADELPHIA ELECTRIC CO.
CROMBY
  150  MW - RETROFIT
COAL   2-U PERCENT SULFUR
UNITED ENGINEERS / PECO
MAGNESIUM OXIDE SCRUBBING
STARTUP   6/80
THE UTILITY PLANS TO RETROFIT ONE OF THE TWO BOILERS AT CROMBY WITH  AN
FGD SYSTEM. HOWEVER, A FINAL DECISION HAS NOT BEEN MADE.  THE PROCESS
BEING GIVEN PRIME CONSIDERATION IS MAGNESIUM OXIDE SCRUBBING, DESIGNED
JOINTLY BY UNITED ENGINEERS AND PHILADELPHIA ELECTRIC.  ENGINEERING
DESIGN WORK IS SCHEDULED TO COMMENCE SOON. TENTATIVE FGD SYSTEM
START-UP IS SCHEDULED FOR JUNE 1980. CURRENTLY, PECO IS CONTINUING
PROCESS EVALUATION STUDIES AT THE EDDYSTONE EXPERIMENTAL UNIT.
PHILADELPHIA ELECTRIC CO.
EDDYSTONE NO.  1A
   120  MW - RETROFIT
COAL 2.5 PERCENT SULFUR
UNITED ENGINEERS / PECO
MAGNESIUM OXIDE SCRUBBING
STARTUP   9/75
REFER TO THE BACKGROUND INFORMATION SECTION IN TABLE 3 OF THIS REPORT.
THE EMISSION CONTROL SYSTEM FOR THIS UNIT CONSISTS OF THREE PARALLEL
SCRUBBING TRAINS FOR THE CONTROL OF PARTICULATE ANQ SULFUR DIOXIDE.
THE C-SIDE SCRUBBING TRAIN INCLUDES AN S02 ABSORBER MODULE IN SERIES
WITH A PARTICULATE SCRUBBER. APPROXIMATELY ONE-THIRD OF THE BOILER FLUE
GAS IS SCRUBBED WITH MAGNESIUM OXIDE SLURRY FOR S02 REMOVAL. THE SPENT
SLURRY IS REGENERATED AT THE ESSEX SULFURIC ACID PLANT IN NEWARK, N.J.
THE REGENERATED MAGOX IS RETURNED TO THE PLANT FOR S02 SCRUBBING SERVICE.
PHILADELPHIA ELECTRIC CO.
EDDYSTONE NO.  IB
  240  MW - RETROFIT
COAL 2.5 PERCENT SULFUR
UNITED ENGINEERS / PECO
MAGNESIUM OXIDE SCRUBBING
STARTUP   6/80
THE INSTALLATION OF S02 SCRUBBERS ON THE BALANCE OF THE FLUE GAS FROM
THIS UNIT WILL FOLLOW PENDING THE OUTCOME OF THE PERFORMANCE OF THE
SCRUBBING UNIT WHICH HAS BEEN INSTALLED AND CURRENTLY OPERATIONAL
ON THE EOOYSTONE NO. 1 UNIT. CURRENTLY, 3 WET PARTICULATE SCRUBBERS ARE
TREATING THE FULL GAS LOAD FROM THIS UNIT. THE PERFORMANCE OF THE MAGOX
UNIT IS DESCRIBED IN THE EDDYSTONE NO. IA FILE CONTAINED IN THIS REPORT.
PHILADELPHIA ELECTRIC CO.
EDDYSTONE NO. 2
  336  MW - RETROFIT
COAL 2.4 PERCENT SULFUR
UNITED ENGINEERS / PECO
MAGNESIUM OXIDE SCRUBBING
STARTUP   6/80
THE UTILITY IS AWAITING PERFORMANCE RESULTS FROM THE EXISTING MGO
SCRUBBER INSTALLED ON UNIT NO. 1 AT THIS STATION BEFORE PROCEEDING
WITH THE DESIGN OF AN FGD SYSTEM FOR THIS COAL-FIRED BOILER. THE PROCESS
BEING GIVEN PRIME CONSIDERATION IS MAGNESIUM OXIDE SCRUBBING DESIGNED
JOINTLY BY UNITED ENGINEERS AND PHILADELPHIA ELECTRIC. ENGINEERING
DESIGN WORK IS SCHEDULED TO COMMENCE SOON. TENTATIVE FGD SYSTEM
START-UP IS SCHEDULED FOR JUNE 1980.
POTOMAC ELECTRIC & POWER
OICKERSON NO. 4
  800  MW - NEW
COAL   2.0 PERCENT SULFUR
NOT SELECTED
NOT SELECTED
STARTUP   5/85
THERE ARE NO FIRM PLANS FOR INSTALLATION OF FGD SYSTEM.  STARTUP DATE OF
BOILER IS PLANNED FOR 1985. THIS UNIT WILL BURN 2 PERCENT SULFUR COAL
WITH A HEATING VALUE OF 11,000 BTU/LB.
POWER  AUTHORITY OF NEW YORK
ARTHUR KILL
  700  MW - NEW
COAL - 3X SULFUR - REFUSE
NOT SELECTED
NOT SELECTED
STARTUP   9/82
THE UTILITY IS CONSIDERING BOTH REGENERABLE AND LIMESTONE SCRUBBING
PROCESSES. FGD TECHNOLOGY IS BEING CONSIDERED FOR A FOSSIL FUEL BURNING
UNIT WHICH WILL EMPLOY COAL AS THE PRIMARY FUEL AND OIL AS BACKUP. REFUSE
WILL BE PROVIDED FOR SUPPLEMENTAL FUEL SUPPLIES. THE PREFERRED PLANT SITE
IS THE ARTHUR KILL FACILITY LOCATED ON STATEN ISLAND. THE PROJECT DESIGN
ENGINEERING FIRM IS SARGENT AND LUNOY. PUBLIC SERVICE COMMISSION HEARINGS
ARE IN PROGRESS. NO DECISIONS WILL BE MADE UNTIL LATE SPRING 1978.
PUBLIC SERVICE CO OF NEW MEX.  CONSTRUCTION
SAN JUAN NO. 1                 WELLMAN LORD
  375  MW - NEW                S02 REDUCTION
COAL   0.8 PERCENT SULFUR      WILL PRECEDE
DAVY POWERGAS/ALLIED CHEMICAL  FOR EACH UNIT
WELLMAN LORD/ALLIED CHEMICAL   STORED ON THE
STARTUP   4/78                 REPORTED HAS
             IS 90% COMPLETE. THIS FGD SYSTEM IS AN INTEGRATION OF THE
             802 RECOVERY PROCESS OF DAVY POWERGAS AND ALLIED CHEMICAL'S
              TO SULFUR PROCESS. A HOT SIDE ELECTROSTATIC PRECIPITATOR
             THE SCRUBBING UNIT. FOUR ABSORBER TOWERS WILL BE INSTALLED
             . THREE WILL CARRY THE FULL LOAD. MOLTEN SULFUR WILL BE
              PLANT SITE. THE INSTRUMENTATION CONTROL PROBLEM PREVIOUSLY
             BEEN SOLVED. START-UP IS SCHEDULED FOR APRIL 1978.
                                                  16

-------
 COMPANY

 POWER STATION
                                       TABLE  2
                            STATUS  OF  FGD  SYSTEMS  AS  OF    01/78

                                                   CURRENT MONTH
PUBLIC SERVICE CO OF NEW MEX.
SAN JUAN NO. 2
  310  MM - RETROFIT
COAL   0.8 PERCENT SULFUR
OAVY POWERGAS/ALLIED CHEMICAL
WELLMAN LORD/ALLIED CHEMICAL
STARTUP   7/78
PUBLIC SERVICE CO OF NEW  MEX.
SAN JUAN NO. 3
  500  MW - NEW
COAL 0.6 PERCENT SULFUR
OAVY POWERGAS
WELLMAN LORD
STARTUP   1/79
                         THE  CONSTRUCTION  OF  THIS  SYSTEM IS NOW UNDERWAY. CONSTRUCTION IS
                         NEARING  COMPLETION.  START-UP IS NOW SCHEDULED FOR JULY 1978. THIS FGD
                         SYSTEM  IS  AN  INTEGRATION  OF  THE WELLMAN LORD S02 RECOVERY PROCESS OF
                         DAVY POWERGAS AND ALLIED  CHEMICAL'S S02 REDUCTION TO SULFUR PROCESS. A
                         HOT  SIDE ELECTROSTATIC  PRECIPITATOR WILL PRECEDE THE SCRUBBING UNIT. FOUR
                         ABSORBER TOWERS WILL BE INSTALLED FOR THIS UNIT. THREE WILL CARRY THE
                         FULL LOAD.  MOLTEN SULFUR  WILL BE STORED ON THE PLANT SITE. START-UP DELAY
                         WAS  CAUSED  BY A BOILER  EXPLOSION.

                         THE  UTILITY HAS SIGNED  A  LETTER-OF-INTENT WITH DAVY POWERGAS FOR
                         ONE  SCRUBBER  MODULE  WHICH WILL BE DESIGNED TO BRING THE UNIT INTO
                         COMPLIANCE  WITH NSPS BY JAN. 1979. THE FGD SYSTEM FOR THE REMAINDER
                         OF  THE  FLUE GAS FROM THIS 500-MW UNIT HAS NOT BEEN SELECTED. PRIMARY
                         PARTICULATE CONTROL  WILL  BE  EFFECTED BY AN UPSTREAM ESP.
PUBLIC SERVICE  CO  OF  NEW  MEX.
SAN JUAN  NO.  4
   500  MW - NEW
COAL 0.8  PERCENT  SULFUR
DAVY POWERGAS
WELLMAN LORD
STARTUP    5/81
                         THE  UTILITY  HAS  PLACED A  HOLD ON FURTHER ENGINEERING DESIGN WORK AT THE
                         PRESENT  TIME.  THE  PROJECTED  START-UP DATE FOR UNIT 4 IS
                         MAY  1981.  THE  WELLMAN LORD S02 RECOVERY  PROCESS WILL BE UTILIZED TO BRING
                         THE  UNIT INTO  COMPLIANCE  WITH NSPS.  AN ESP WILL BE PROVIDED UPSTREAM OF
                         THE  FGD  SYSTEM FOR PRIMARY PARTICULATE CONTROL.
 PUBLIC  SERVICE  OF  INDIANA
 GIBSON  5
   650   MW  -  NEW
 COAL  3.3 PERCENT  SULFUR
 NOT SELECTED
 NOT SELECTED
 STARTUP   0/82
                         THE UTILITY  IS IN THE PROCESS OF  PREPARING SPECIFICATIONS. SCHEDULED
                         START-UP OF  THIS 650 MW UNIT IS 1982.
 SALT  RIVER  PROJECT
 CORONADO NO.l
   350  MW - NEW
 COAL  1.0 PERCENT SULFUR (MAX)
 PULLMAN KELLOGG
 LIMESTONE SCRUBBING
 STARTUP   4/79
                         THIS NEW UNIT WILL BURN LOW SULFUR WESTERN COAL.  A MAXIMUM OF 80X OF THE
                         FLUE GAS WILL BE SCRUBBED TO MEET SULFUR DIOXIDE  EMISSION REGULATIONS.
                         PULLMAN/KELLOGG WILL DESIGN AND FABRICATE TWO WEIR HORIZONTAL
                         CROSSFLOW SCRUBBER MODULES, WHICH WILL UTILIZE LIMESTONE SLURRY FOR
                         302 CONTROL.  THE SYSTEM WILL UTILIZE RUBBER-LINED SLURRY RECYCLE PUMPS,
                         EACH RATED AT 9800 GPM, RIGIFLAKE-LINED SCRUBBER  MODULES, VERTICAL HEIL
                         DEMISTERS, AND A MINIMUM OF 20 PERCENT REHEAT. THE SLUDGE WILL BE PONDED.
                         THE FOUNDATION IS COMPLETED AND STRUCTURAL WORK HAS COMMENCED.
 SALT RIVER PROJECT
 CORONADO NO.2
   350  MW - NEW
 COAL 1.0 PERCENT SULFUR (MAX)
 PULLMAN KELLOGG
 LIMESTONE SCRUBBING
 STARTUP   «/80
                         THIS NEW UNIT WILL BURN LOW SULFUR WESTERN COAL.  A MAXIMUM OF SOX OF THE
                         FLUE GAS WILL BE SCRUBBED TO MEET SULFUR DIOXIDE  EMISSION REGULATIONS.
                         PULLMAN/KELLOGG WILL DESIGN AND FABRICATE TWO WEIR HORIZONTAL
                         CRUSSFLOW SCRUBBER MODULES, WHICH WILL UTILIZE LIMESTONE SLURRY FOR
                         302 CONTROL. THE SYSTEM WILL UTILIZE RUBBER-LINED SLURRY RECYCLE PUMPS,
                         EACH RATED AT 9800 GPM, RIGIFLAKE-LINED SCRUBBER  MODULES, VERTICAL HEIL
                         DEMISTERS  AND A MINIMUM OF 20 PERCENT REHEAT. THE SLUDGE WILL BE PONDED.
                         FOUNDATION WORK HAS BEEN COMPLETED,  STRUCTURAL STEEL WORK HAS COMMENCED.
 SALT  RIVER PROJECT
 CORONADO NO.3
   350  MW - NEW
 COAL  1.0 PERCENT SULFUR (MAX)
 NOT SELECTED
 LIMESTONE SCRUBBING
 STARTUP   0/97
                         THIS NEW UNIT WILL BURN LOW SULFUR WESTERN COAL.  80 PERCENT OF THE
                         GAS WILL BE SCRUBBED TO MEET SULFUR DIOXIDE EMISSION REGULATIONS.
                         THE UTILITY IS CURRENTLY CONSIDERING THE INSTALLATION OF TWO HORIZONTAL
                         CROSSFLOW SCRUBBING MODULES EMPLOYING A LIMESTONE SCRUBBING SOLUTION
                         TO REMOVE S02 FROM THE FLUE GAS.   SCHEDULED COMMERCIAL OPERATION
                         DATE IS 1967.  PLANS FOR AN EMISSION CONTROL SYSTEM HAVE NOT
                         BEEN FINALIZED. SLUDGE WILL PROBABLY BE PONDED.
 SOUTH CAROLINA  PUBLIC SERVICE
 WINYAH NO.  2
   260
 COAL
 MW - NEW
1.0 PERCENT SULFUR
 BABCOCK  *  WILCOX
 LIMESTONE  SCRUBBING
 STARTUP    7/77
REFER TO THE BACKGROUND INFORMATION SECTION IN TABLE 3 OF THIS REPORT.
THE EMISSION CONTROL SYSTEM FOR THIS UNIT CONSISTS OF A 100X CAPACITY ESP
FOLLOWED BY A SOX CAPACITY LIMESTONE FGD SYSTEM. ONE FGD MODULE, CONSIST-
ING OF A VENTURI SCRUBBER AND TRAY TOWER ABSORBER, REMOVES 70* OF THE
INLET S02. REHEAT IS SUPPLIED BY THE FLUE SAS BYPASS. THE SCRUBBING
WASTES ARE DISCHARGED TO AN ON-SITE, UNLINED DIKED POND. THE NO. 2 UNIT
COMMENCED INITIAL OPERATIONS IN JULY 1977. THE ACCEPTANCE TEST FOR COM-
MERCIAL CERTIFICATION WAS SUCCESSFULLY COMPLETED IN DECEMBER 1977.
                                                   17

-------
 COMPANY

 POWER STATION
              TABLE 2
   STATUS OF FGD SYSTEMS AS OF
                                 01/78
                                                         CURRENT MONTH
SOUTH CAROLINA PUBLIC SERVICE
WINYAH NO. 3
  300  MW - NEW
COAL 2.3 PERCENT SULFUR
NOT SELECTED
NOT SELECTED
STARTUP   0/80
SANTEE COOP, AND SOUTH CAROLINA PUBLIC SERVICE AWARDED RILEY STOKER
A CONTRACT TO DESIGN, FABRICATE AND ERECT A NEW STEAM GENERATING UNI
THE COAL-FIRED DRY-BOTTOM TURBO-FIRED FURNACE WILL PRODUCE STEAM FOR  THE
300 MW TURBINE GENERATOR. BOX OF THE FLUE GAS WILL BE SCRUBBED FOR S02,
20X WILL BE BYPASSED FOR REHEAT. THE COAL BURNED HAS A 11,500
BTU/LB AND 2.3X SULFUR. STARTUP IS SCHEDULED FOR THE SUMMER OF 1980.  THE
FGD SYSTEM CONTRACT IS UP FOR BIDS.
SOUTHERN ILLINOIS POWER COOP
MARION NO. 4
  18U  MW - NEW
COAL   a.5-5.0 PERCENT SULFUR
BABCOCK & WILCOX
LIMESTONE SCRUBBING
STARTUP   6/78
THE EMISSION CONTROL SYSTEM FOR THIS NEW COAL-FIRED BOILER CONSISTS OF  AN
ESP FOR PARTICULATE CONTROL FOLLOWED BY 2 SPRAY TOWERS FOR 502 CONTROL.
LIMESTONE SLURRY WILL BE USED AS THE SCRUBBING REAGENT. SIPC IS NOT PLAN-
NING TO UTILIZE FLUE GAS REHEAT AND IS CURRENTLY PLANNING ON BRICK LINING
FOR THE STACK. SIPC INTENDS TO USE A LANDFILL WITH ASH STABILIZATION OF
WASTE FOR SLUDGE DISPOSAL. CURRENTLY, CONSTRUCTION IS 75 PERCENT COMPLETE
ON THE UNIT AND FGD SYSTEM.
SOUTHERN  INDIANA GAS&ELECTRIC
A.B. BROWN NO.l
  250  MW - NEW
COAL 3.75 PERCENT SULFUR
FMC CORPORATION
DOUBLE ALKALI SCRUBBING
STARTUP   1/79
THE UTILITY HAS AWARDED A CONTRACT TO FMC FOR THE INSTALLATION OF A
DOUBLE ALKALI SCRUBBING SYSTEM UTILIZING SODA ASH AND LYE. THIS UNIT IS
A PART OF A NEW POWER STATION LOCATED IN WEST FRANKLIN, INDIANA. THE
SYSTEM WILL PRODUCE FILTER CAKE AS A WASTE PRODUCT WHICH WILL BE DIS-
POSED OF IN AN ON-SITE LANDFILL. THE PARTICULATE EMISSIONS WILL BE CON-
TROLLED BY A BUELL-ENVIROTECH COLD-SIDE ESP. THE CONSTRUCTION WORK AND
ENFINEERING IS 20X COMPLETE.
 SOUTHERN MISSISSIPPI ELECTRIC
 R.D. MORROW NO.l
   180  MW - NEW
 COAL 1.0 PERCENT SULFUR
 RILEY STOKER / ENVIRONEERING
 LIMESTONE SCRUBBING
 STARTUP   5/78
CONSTRUCTION OF THE WET LIMESTONE SCRUBBING SYSTEM IS 50 PERCENT COM-
PLETE. PARTICULATES WILL BE CONTROLLED BY A HIGH-EFFICIENCY ESP UPSTREAM
OF THE SCRUBBING SYSTEM. DESIGN SULFUR DIOXIDE AND PARTICULATE REMOVAL
EFFICIENCIES ARE 85 AND 99.6 PERCENT, RESPECTIVELY. A WATER SPRAY HAS
BEEN ADDED IN THE BY-PASS DUCT TO PROTECT THE LINER FROM TEMPERATURE
EXCURSION, SCRUBBER SLUDGE WILL BE STABILIZED WITH FLYASH AND DISPOSED ON
THE PLANT SITE.
 SOUTHERN MISSISSIPPI ELECTRIC
 R.O. MORROW  NO.2
   180  MW  -  NEW
 COAL 1.0 PERCENT SULFUR
 RILEY STOKER / ENVIRONEERING
 LIMESTONE  SCRUBBING
 STARTUP    8/78
CONSTRUCTION OF THE WET LIMESTONE SCRUBBING SYSTEM IS 50 PERCENT COM-
PLETE. PARTICULATES WILL BE CONTROLLED BY A HIGH-EFFICIENCY ESP UPSTREAM
OF THE SCRUBBING SYSTEM. DESIGN SULFUR DIOXIDE AND PARTICULATE REMOVAL
EFFICIENCIES ARE 85 AND 99.6 PERCENT, RESPECTIVELY. A WATER SPRAY HAS
BEEN ADDED IN THE BY-PASS DUCT TO PROTECT THE LINER FROM TEMPERATURE
EXCURSION. SCRUBBER SLUDGE WILL BE STABILIZED WITH FLYASH AND DISPOSED ON
THE PLANT SITE.
 SPRINGFIELD CITY UTILITIES
 SOUTHWEST NO.  1
  200   MW - NEW
 COAL 3.5 PERCENT SULFUR
 UNIVERSAL OIL  PRODUCTS
 LIMESTONE SCRUBBING
 STARTUP   4/77
REFER TO THE BACKGROUND INFORMATION SECTION IN TABLE 3 OF THIS REPORT.
THE EMISSION CONTROL SYSTEM FOR THIS NEW COAL-FIRED UNIT CONSISTS OF A
FOUR-FIELD HIGH EFFICIENCY ESP (99.6X DESIGN) AND 2 TURBULENT CONTACT AB-
SORBER MODULES (BOX DESIGN) FOR THE CONTROL OF PARTICULATES AND S02. BOTH
THE ESP AND LIMESTONE FGD SYSTEM ARE SUPPLIED BY UOP. THE SCRUBBING
WASTES ARE DEWATERED BY A ROTARY DRUM VACUUM FILTER AND THE FILTER CAKE IS
HAULED AWAY TO A LANDFILL. INITIAL OPERATION OF THE FGD SYSTEM OCCURRED IN
APRIL 77. IN SEPT. 77, THE UNIT SUCCESSFULLY COMPLETED COMPLIANCE TESTING.
 SPRINGFIELD WATER  LIGHT4POWER A CONTRACT HAS BEEN AWARDED TO RESEARCH COTTRELL FOR THE  INSTALLATION  OF
 DALLMAN  NO.  3
   190  MW -  NEW
 COAL   3.0-4.3 PERCENT SULFUR
 RESEARCH COTTRELL
 LIMESTONE SCRUBBING
 STARTUP   7/80
A LIMESTONE SCRUBBING SYSTEM. REQUIRED SULFUR DIOXIDE REMOVAL EFFICIENCY
IS 90 PERCENT. A SLUDGE DISPOSAL STRATEGY HAS NOT BEEN FINALIZED, BUT
THE UTILITY IS CONSIDERING EITHER PONDING OR LANDFILL. SCRUBBER CONSTRUC-
TION OF THE FGD SYSTEM SHOULD COMMENCE IN LATE 1978. FGD START-UP IS
SCHEDULED FOR JULY 1980. BOILER OPERATION IS SCHEDULED TO COMMENCE IN
JUNE 1978.
TENNESSEE VALLEY AUTHORITY
SHAWNEE N0.10A
   10  MW - RETROFIT
COAL 2.9 PERCENT SULFUR
UNIVERSAL OIL PRODUCTS
LIME/LIMESTONE SCRUBBING
STARTUP   4/72
REFER TO BACKGROUND INFORMATION SECTION IN TABLE 3 OF THIS REPORT. THIS
TURBULENT CONTACT ABSORBER(TCA) LIME/LIMESTONE SCRUBBING SYSTEM HAS BEEN
OPERATIONAL SINCE APRIL 1972. THIS TEST PROGRAM IS FUNDED BY THE EPA.
TVA IS THE CONSTRUCTOR AND FACILITY OPERATOR. THE BECHTEL CORP. OF SAN
FRANCISCO IS THE MAJOR CONTRACTOR, TEST DIRECTOR, AND REPORT WRITER.
DURING THE REPORT PERIOD, OPERATIONS WERE CONDUCTED WITH LIMESTONE
SLURRY CIRCULATING THROUGH THE UNIT. FORCED OXIDATION ON FLY ASH-LADEN
FLUE GAS WAS EVALUATED.
                                                  18

-------
 COMPANY

 POWER STATION
              TABLE 2
   STATUS OF F60 SYSTEMS AS OF
       01/78

CURRENT MONTH
TENNESSEE VALLEY AUTHORITY
SHAWNEE N0.10B
   10  MM - RETROFIT
COAL 2,9 PERCENT SULFUR
CHEMICO
LIME/LIMESTONE SCRUBBING
STARTUP   4/72
REFER TO BACKGROUND INFORMATION SECTION IN TABLE 3 OF THIS REPORT. THIS
VENTURI/SPRAY TOWER LIME/LIMESTONE SCRUBBING SYSTEM HAS BEEN OPERATIONAL
SINCE APRIL 1972. THIS TEST PROGRAM IS FUNDED BY THE EPA. TVA IS THE
CONSTRUCTOR AND FACILITY OPERATOR. THE BECHTEL CORP. OF SAN FRANCISCO IS
THE MAJOR CONTRACTOR, TEST DIRECTOR, AND REPORT WRITER. DUHING THE REPORT
PERIOD. FORCED OXIDATION WAS EVALUATED ON FLY ASH-FREE FLUE GAS WITH
LIME SLURRY AS THE SCRUBBING AGENT.
TENNESSEE VALLEY  AUTHORITY
WIDOWS CREEK NO.  7
  575  MW - RETROFIT
COAL 3.7 PERCENT  SULFUR
COMBUSTION ENGINEERING
LIMESTONE SCRUBBING
STARTUP   O/ 0
TENNESSEE VALLEY AUTHORITY ANNOUNCED DURING THE REPORT PEHIOO THAT A CON-
TRACT HAS BEEN AWARDED TO COMBUSTION ENGINEERING FOR A LIMESTONE SLURRY
SPRAY TOWER FGO SYSTEM. THE FGD SYSTEM WILL TREAT HIGH SULFUR COAL FLUE
GAS. THE SPRAY TOWER ABSORBERS WILL BE CONSTRUCTED OF 317 L STAINLESS
STEEL. THE NO. 7 UNIT FIRES COAL WITH THE SAME CHARACTERISTICS AS THE COAL
FIRED IN THE NO. 8 UNIT.
 TENNESSEE  VALLEY  AUTHORITY
 WIDOWS CREEK  NO.  8
  550  MW  - RETROFIT
 COAL   3.7 PERCENT  SULFUR
 TENNESSEE  VALLEY  AUTHORITY
 LIMESTONE  SCRUBBING
 STARTUP    5/77
REFER TO THE BACKGROUND INFORMATION SECTION IN TABLE 3 OF THIS REPORT.
THE EMISSION CONTROL SYSTEM FOR THIS 550-MW COAL-FIRED POWER-GENERATING
UNIT CONSISTS OF EXISTING ELECTROSTATIC PRECIPITATORS FOLLOWED BY FOUR
PARALLEL SCRUBBING TRAINS, EACH CAPABLE OF HANDLING 25 PERCENT OF THE
BOILER FLUE GAS FROM UNIT NO. 8. EACH  TRAIN INCLUDES A RECTANGULAR-
THROAT VENTURI SCRUBBER AND A GRIO-TOWER ABSORBER SUPPLIED BY POLYGON.
THE GRID TOWER CAN BE CONVERTED TO A MOBILE-BED TOWER IF GREATER S02 RE-
MOVAL IS REQUIRED.
 TEXAS  MUNICIPAL  POWER  AGENCY
 GIBBONS  CREEK  UNIT  NO.  1
   400   MW  -  NEW
 LIGNITE  -  1.06 PERCENT  SULFUR
 COMBUSTION ENGINEERING
 LIMESTONE  SCRUBBING
 STARTUP    1/82
COMBUSTION ENGINEERING WAS AWARDED A CONTRACT TO DESIGN AND SUPPLY
 A 400 MW LIGNITE-FIRED BOILER, ESP, AND FGD SYSTEM AT GIBBONS CREEK
STEAM ELECTRIC STATION UNIT NO. 1. THE BOILER WILL BURN l.ObZ SULFUR
LIGNITE. FLUE GAS WILL BE CLEANED OF PARTICULATES BY A COLD-SIDE ESP
199.73X EFFICIENCY). S02 WILL BE REMOVED BY 3 SPRAY TOWER MODULES UTILI-
ZING A LIMESTONE SLURRY (72.5 TO 87.5X EFFICIENCY). COMMERCIAL START-UP
HAS BEEN SET FOR JANUARY 1982.
 TEXAS POWER AND LIGHT  CO.
 SANDOW NO.4
   545  MW - NEW
 LIGNITE
 COMBUSTION  ENGINEERING
 LIMESTONE SCRUBBING
 STARTUP   7/80
COMBUSTION ENGINEERING HAS BEEN CHOSEN AS THE BOILER AND FGD VENDOR FOR
THIS UNIT. BOILER CONSTRUCTION BEGAN ON SEPTEMBER 9, 1977. THE PARTI-
CULATE REMOVAL IS TO TAKE PLACE ON THE COLD-SIDE OF THE AIR HEATER.
SOME PORTION OF FLUE-GAS WILL BYPASS SCRUBBER FOR REHEAT. THE SPENT
SLURRY WILL BE PONDED AND WATER RECYCLED. FGD CONSTRUCTION IS SCHEDULED
TO BEGIN NOVEMBER 1978.
 TEXAS POWER AND LIGHT CO.
 TWIN OAKS NO.  1
   750  MW - NEW
 LIGNITE
 NOT SELECTED
 NOT SELECTED
 STARTUP   8/83
THIS UNIT WILL BE JOINTLY OWNED BY TP&L AND ALCOA.  A FIRM DECISION HAS
NOT BEEN MADE WHETHER TO INSTALL FGD FACILITIES. THIS IS PRIMARILY
DUE TO THE FACT THAT SUCH A DECISION IS NOT YET REQUIRED IN THE
UTILITIES PLANNING TIMETABLE.
 TEXAS POWER AND LIGHT CO.
 TWIN OAKS NO.  2
   750  MW - NEW
 LIGNITE
 NOT SELECTED
 NOT SELECTED
 STARTUP   9/84
THIS UNIT WILL BE JOINTLY OWNED BY TP&L AND ALCOA.  A FIRM DECISION HAS
NOT BEEN MADE WHETHER TO INSTALL FGD FACILITIES. THIS IS PRIMARILY
DUE TO THE FACT THAT SUCH A DECISION IS NOT YET REQUIRED IN THE
UTILITIES PLANNING TIMETABLE.
 TEXAS UTILITIES CO.
 FOREST GROVE NO. 1
   750  MW - NEW
 LIGNITE
 NOT SELECTED
 NOT SELECTED
 STARTUP   0/81
TEXAS UTILITIES REPORTED THAT A NEW 750-MW LIGNITE-FIRED UNIT IS  IN
THE EARLY PLANNING STAGE FOR THE FOREST GROVE STATION IN ATHENS,  TEXAS.
START-UP IS SCHEDULED FOR LATE 1981.  THE BOILER WILL BE SUPPLIED
BY THE BABCOCK & WILCOX COMPANY.
                                                  19

-------
 COMPANY

 POWER STATION
              TABLE 2
   STATUS OF FGO SYSTEMS AS OF
                                 01/78
                                                         CURRENT MONTH
TEXAS UTILITIES CO.
MARTIN LAKE NO. 1
  793  MW - NEW
COAL   1.0 PERCENT SULFUR
RESEARCH COTTRELL
LIMESTONE SCRUBBING
STARTUP   8/77
THIS NEW 793-MW POWER
0.9X SULFUR (AVG) AND
UNIT HAS BEEN EQUIPPED
COLD-SIDE ESP'S AND A
TRELL. THE FGD SYSTEM
TREAT 75X OF THE TOTAL
FOR REHEAT. TOTAL S02
WASTES ARE STABILIZED
GENERATING UNIT FIRES TEXAS LIGNITE WHICH CONTAINS
6.OX ASH (AVG.). IN ORDER TO MEET FEDERAL NSPS THt
 WITH AN EMISSION CONTROL SYSTEM WHICH INCLUDES
LIMESTONE FGO SYSTEM BOTH SUPPLIED BY RESEARCH-COT-
CONSISTS OF 6 PACKED/SPRAY TOWER ABSORBERS WHICH
 BOILER FLUE GAS. THE REMAINING FLUE GAS IS BYPASSED
REMOVAL EFFICIENCY IS 70.5X. THE FLUE GAS CLEANING
AND DISPOSED IN AN ON-SITE, LINED POND.
TEXAS UTILITIES CO.
MARTIN LAKE NO. 2
  793  MW - NEW
COAL   1.0 PERCENT SULFUR
RESEAHCH COTTRELL
LIMESTONE SCRUBBING
STARTUP   2/78
TEXAS UTILITIES CO.
MARTIN LAKE NO. 3
  793  MW - NEW
COAL 1.0 PERCENT SULFUR
RESEARCH COTTRELL
LIMESTONE SCRUBBING
STARTUP  12/76
THIS NEW 793-MW POWER GENERATING UNIT WILL FIRE TEXAS LIGNITE CONTAINING
0.9X SULFUR (AVG.) AND 8X ASH (AVG.). TO MEET FEDERAL NSPS, THE UNIT WILL
BE EQUIPPED WITH AN EMISSION CONTROL SYSTEM CONSISTING OF COLO-SIDE ESP S
AND A LIMESTONE FGD SYSTEM, BOTH SUPPLIED BY RESEARCH-COTTRELL. THE FGD
SYSTEM CONSISTS OF 6 PACKED/SPRAY TOWER ABSORBERS WHICH WILL TREAT 75X OF
THE TOTAL BOILER FLUE GAS. THE REMAINING GAS WILL BE BYPASSED FOR REHEAT.
TOTAL DESIGN S02 REMOVAL EFFICIENCY IS 70.5X. THE FLUE GAS CLEANING WASTES
WILL BE STABILIZED AND DISPOSED IN AN ON-SITE, LINED POND.

THIS NEW 793-MW POWER GENERATING UNIT WILL FIRE TEXAS LIGNITE CONTAINING
0.9X SULFUR (AVG.) AND 8X ASH (AVG.). TO MEET FEDERAL NSPS, THE UNIT WILL
BE EQUIPPED WITH AN EMISSION CONTROL SYSTEM CONSISTING OF COLD-SIDE ESP'S
AND A LIMESTONE FGD SYSTEM, BOTH SUPPLIED BY RESEARCH-COTTRELL. THE FGD
SYSTEM CONSISTS OF 6 PACKED/SPRAY TOWER ABSORBERS WHICH WILL TREAT 75X OF
THE TOTAL BOILER FLUE GAS. THE REMAINING GAS WILL BE BYPASSED FOR REHEAT.
TOTAL DESIGN 302 REMOVAL EFFICIENCY IS 70.5X. THE FLUE GAS CLEANING WASTES
WILL BE STABILIZED AND DISPOSED IN AN ON-SITE, LINED POND.
 TEXAS UTILITIES CO.
 MARTIN LAKE NO. a
  793  MW - NEW
 COAL 1.0 PERCENT SULFUR
 RESEARCH COTTRELL
 LIMESTONE SCRUBBING
 STARTUP  11/82
THE CONTRACT FOR THIS FGD SYSTEM HAS BEEN AWARDED TO RESEARCH-COTTRELL.
THE BOILER IS NOW BEING ERECTED. START-UP IS SCHEDULED FOR THE FOURTH
QUARTER OF 1982.
 TEXAS UTILITIES CO.
 MONTICELLO NO.3
   750  MW - NEW
 LIGNITE  1.5 PERCENT SULFUR
 CHEMICO
 LIMESTONE SCRUBBING
 STARTUP   2/76
THE EMISSION CONTROL SYSTEM FOR THIS UNIT CONSISTS OF A HIGH EFFICIENCY
ESP AND A LIMESTONE FGD SYSTEM. THE ESP (POLLUTION CONTROL-WALTHER) IS
PROVIDED FOR PRIMARY PARTICULATE CONTROL (99.56X). THE FGD SYSTEM CONSISTS
OF LIMESTONE SCRUBBING SPRAY TOWERS (CHEMICO) AND WILL PROVIDE PRIMARY
S02 CONTROL (7«X). THE FGD SYSTEM IS DESIGNED TO TREAT APPROXIMATELY 3MM
SCFM OF FLUE GAS RESULTING FROM COAL WITH 1.5X SULFUR, 18.9X ASH AND
O.OaX CI. THE FLUE GAS CLEANING WASTES WILL BE STABILIZED AND DISPOSED IN
AN ON-SITE, LINED POND. CURRENTLY, INSTALLATION IS NEARING COMPLETION.
 UNITED  POWER ASSOCIATION
 COAL CREEK NO.  1
   545   MW • NEW
 LIGNITE  - 0.63  PERCENT SULFUR
 COMBUSTION ENGINEERING
 LIME SCRUBBING
 STARTUP   11/78
THE CONTRACT FOR THIS SCRUBBING SYSTEM HAS BEEN AWARDED TO COMBUSTION
ENGINEERING FOR THE INSTALLATION OF LIME FGD SYSTEMS ON UNITS NOS.l AND 2
AT THIS STATION. THE SCRUBBING SYSTEM FOR EACH BOILER WILL CONSIST OF
4 SPRAY TOWER ABSORBER MODULES FOR REMOVING 302 FROM THE FLUE GAS.
ELECTROSTATIC PHECIPITATORS WILL BE INSTALLED UPSTREAM OF EACH SCRUBBING
SYSTEM. FGD CONSTRUCTION BEGAN IN EARLY AUGUST 1977.
 UNITED  POWER  ASSOCIATION
 COAL CREEK NO. 2
   545   MW - NEW
 LIGNITE  • 0.63 PERCENT SULFUR
 COMBUSTION ENGINEERING
 LIME SCRUBBING
 STARTUP  11/79
THE CONTRACT FOR THIS SCRUBBING SYSTEM HAS BEEN AWARDED TO COMBUSTION
ENGINEERING FOR THE INSTALLATION OF LIME FGD SYSTEMS ON UNITS NOS. 1 AND
2 AT THIS STATION. THE SCRUBBING SYSTEM FOR EACH BOILER WILL CONSIST OF
4 SPRAY TOWER ABSORBER MODULES FOR REMOVING S02 FROM THE FLUE GAS.
ELECTROSTATIC PRECIPITATORS WILL BE INSTALLED UPSTREAM OF EACH SCRUBBING
SYSTEM. FGD CONSTRUCTION BEGAN IN AUGUST 77. THE START-UP TARGET
DATE MAY NOT BE ACHIEVED DUE TO DELAYS IN CONSTRUCTION SCHEDULE.
UTAH POWER » LIGHT CO.
EMERY NO.I
  400  MW - NEW
COAL 0.5 PERCENT SULFUR
CHEMICO
LIME SCRUBBING
STARTUP  12/78
A CONTRACT HAS BEEN AWARDED TO THE CHEMICO AIR POLLUTION DIVISION FOR
A PEBBLE LIME WET SCRUBBING SYSTEM ON THIS NEW UNIT. THE SCRUBBING
SYSTEM IS DESIGNED TO OPERATE IN AN OPEN WATER LOOP MODE WITH AN S02
REMOVAL EFFICIENCY OF 80 PERCENT FOR LOW SULFUR UTAH COAL. PRIMARY
PARTICULATE CONTROL WILL BE PROVIDED BY AN ESP UPSTREAM OF THE SCRUBBERS.
THE SCRUBBER SLUDGE WILL BE STABILIZED WITH FLYASH AND DISPOSED ON THE
PLANT SITE.  THE A-E DESIGN FIRM FOR THIS PROJECT IS STEARNS-ROGER.
CONSTRUCTION IS UNDERWAY ON THE FGD SYSTEM FOR THIS UNIT.
                                                  20

-------
 COMPANY

 POWER STATION
UTAH POWER & LIGHT CO.
HUNTIN6TON NO.l
  415  MW - NEW
COAL  0.5 PERCENT SULFUR
CHEMICO
LIME SCRUBBING
STARTUP   4/78
                                             TABLE a
                                  STATUS OF F60 SYSTEMS AS OF
01/78
                                                         CURRENT MONTH
                               A CONTRACT HAS BEEN AWARDED TO CHEMICO AIR POLLUTION DIVISION FOR
                               A LIME SCRUBBING SYSTEM ON THIS NEW UNIT. SITE PREPARATION AND CONSTRUC-
                               TION IS NEARING COMPLETION. THE STATE OF UTAH REGULATIONS REQUIRE THE
                               BEST AVAILABLE AND MOST COST EFFECTIVE TECHNOLOGY FOR SULFUR DIOXIDE
                               REMOVAL. PRIMARY PARTICULATE REMOVAL WILL BE PROVIDED BY AN ESP INSTALLED
                               UPSTREAM OF THE WET SCRUBBING SYSTEM. THE TURNKEY COST FOR THE TWO FGD
                               SYSTEMS (EMERY NO.l AND HUNTINGTON NO.l) IS S29 MM AND $26 MM RESPECTIVE-
                               LY.
VIRGINIA ELECTRIC AND  POWER CO  THE  UTILITY  IS  PRESENTLY CONSIDERING BOTH DESULFURIZATION  AND  THE USE OF
MT. STORM
 1147  MW • RETROFIT
COAL
NOT SELECTED
NOT SELECTED
STARTUP   O/ 0
                               LOW SULFUR COAL. A DESULFURIZATION SYSTEM WOULD TREAT 69 PERCENT OF THE
                               FLUE GAS FROM THREE BOILERS. CONSTRUCTION AND STARTUP DATES ARE CON-
                               SIDERED INDEFINITE AT THIS TIME.
WISCONSIN  POWER  & LIGHT  CO.
COLUMBIA NO.  
-------
                      CONTENTS
                                 TABLE 3
       UTILITY COMPANY              SIZE
        POWER STATION           RETROFIT

ARIZONA PUBLIC SERVICE               US
CHOLLA NO 1

COLUMBUS & SOUTHERN OHIO ELEC.       400
CONESVILLE NO 5

OUQUESNE LIGHT                       510
ELRAMA POWER STATION

OUQUESNE LIGHT                       410
PHILLIPS POWER STATION

INDIANAPOLIS POWER & LIGHT CO.       530
PETERSBURG NO 3

KANSAS CITY POWER & LIGHT            140
HAWTHORN NO. 3

KANSAS CITY POWER & LIGHT            100
HAWTHORN NO. 4

KANSAS CITY POWER & LIGHT            620
LA CYGNE NO 1

KANSAS POWER & LIGHT                 185
LAWRENCE NO 4

KANSAS POWER & LIGHT                 400
LAWRENCE NO 5

KENTUCKY UTILITIES                    64
GREEN RIVER NOS. 1  1  AND 3

LOUISVILLE GAS & ELECTRIC            178
CANE HUN NO 4

LOUISVILLE GAS & ELECTRIC             65
PADDYS RUN NO 6

MINNKOTA POWER COOPERATIVE           450
MILTON R.  YOUNG NO. 2

MONTANA POWER CO.                    360
COLSTRIP NO 1

MONTANA POWER CO.                    360
COLSTRIP NO 2

NEVADA POWER                         125
REID GARDNER NO 1

NEVADA POWER                         125
REID GARDNER NO 2

NEVADA POWER                         125
REID GARDNER NO 3

NORTHERN INDIANA PUS SERVICE         115
O.H. MITCHELL NO.11

NORTHERN STATES POWER CO.            710
SHERBURNE COUNTY STATION NO.l

NORTHERN STATES POWER CO.            710
SHERBURNE COUNTY STATION NO.2

PENNSYLVANIA POWER CO.               825
BRUCE MANSFIELD NO. 1

PENNSYLVANIA POWER CO.               625
BRUCE MANSFIELD NO. 2

PHILADELPHIA ELECTRIC CO.            120
EDDYSTONE NO. 1A
OF FGO  PROCESS/VENDOR                  PAGE NO.
  UNIT (MW)

     RESEARCH COTTRELL
     LIMESTONE SCRUBBING                 24

     UNIVERSAL OIL PRODUCTS
     LIME SCRUBBING                      29

     CHEMICO
     LIME SCRUBBING                      33

     CHEMICO
     LIME SCRUBBING                      38

     UNIVERSAL OIL PRODUCTS
     LIMESTONE SCRUBBING                 43

     COMBUSTION ENGINEERING
     LIME SCRUBBING                      45

     COMBUSTION ENGINEERING
     LIME SCRUBBING                      50

     BABCOCK & WILCOX
     LIMESTONE SCRUBBING                 55

     COMBUSTION ENGINEERING
     LIMESTONE SCRUBBING                 60

     COMBUSTION ENGINEERING
     LIMESTONE SCRUBBING                 64

     AMERICAN AIR FILTER
     LIME SCRUBBING                      68

     AMERICAN AIR FILTER
     LIME SCRUBBING                      73

     COMBUSTION ENGINEERING
     LIME SCRUBBING                      77

     ADL/COMBUSTION EQUIP ASSOCIATE
     LIME/ALKALINE FLYASH SCRUBBING      81

     AOL/COMBUSTION EQUIP ASSOCIATE
     LIME/ALKALINE FLYASH SCRUBBING      84

     ADL/COMBUSTIUN EQUIP ASSOCIATE
     LIME/ALKALINE FLYASH SCRUBBING      85

     ADL/COMBUSTION EQUIP ASSOCIATE
     SODIUM CARBONATE SCRUBBING          88

     ADL/COMBUSTION EQUIP ASSOCIATE
     SODIUM CARBONATE SCRUBBING          93

     ADL/COMBUSTION EQUIP ASSOCIATE
     SODIUM CARBONATE SCRUBBING          99

     DAVY POWERGAS/ALLIED CHEMICAL
     WELLMAN LORD/ALLIED CHEMICAL       104

     COMBUSTION ENGINEERING
     LIMESTONE SCRUBBING                107

     COMBUSTION ENGINEERING
     LIMESTONE SCRUBBING                11 1

     CHEMICO
     LIME SCRUBBING                     114

     CHEMICO
     LIME SCRUBBING                     120

     UNITED ENGINEERS / PECO
     MAGNESIUM OXIDE SCRUBBING          123
                                           22

-------
                      CONTENTS - TABLE 3
       UTILITY COMPANY
        POWER STATION

SOUTH CAROLINA PUBLIC SERVICE
WINYAH NO. 2

SPRINGFIELD CITY UTILITIES
SOUTHWEST NO. J

TENNESSEE VALLEY AUTHORITY
SHAWNEE N0.10A

TENNESSEE VALLEY AUTHORITY
SHAWNEE NO.106

TENNESSEE VALLEY AUTHORITY
WIDOWS CREEK NO. 6

TEXAS UTILITIES CO.
MARTIN LAKE NO. 1
    SIZE OF FGD  PROCESS/VENDOR
RETROFIT   UNIT (Mw)

     280      BABCOCK & HILCOX
              LIMESTONE SCRUBBING

     £00      UNIVERSAL OIL PRODUCTS
              LIMESTONE SCRUBBING

      10      UNIVERSAL OIL PRODUCTS
              LIME/LIMESTONE SCRUBBING

      10      CHEMICO
              LIME/LIMESTONE SCRUBBING

     550      TENNESSEE VALLEY AUTHORITY
              LIMESTONE SCRUBBING

     793      RESEARCH COTTRELL
              LIMESTONE SCRUBBING
PAGE NO.


127


130


133


134


141


144
                                                  23

-------
                  TABLE 3
PERFORMANCE DESCRIPTION FOR OPERATIONAL F6D SYSTEMS THROUGH  01/78
 UTILITY NAME


 UNIT NAME


 UNIT LOCATION


 UNIT RATING


 FUEL CHARACTERISTICS


 FGO VENDOR


 PROCESS


 NEW OR RETROFIT


 START UP DATE


 FGO STATUS


 EFFICIENCY,
   PARTICULATES
 ARIZONA  PUBLIC  SERVICE


 CHOLLA  NO 1


 JOSEPH  CITY  ARIZONA


  115 MW


 COAL   0.44-1  PERCENT  SULFUR


 RESEARCH COTTRELL


 LIMESTONE SCRUBBING


 RETROFIT


 10/73


 OPERATIONAL



 99.7 PERCENT
   soe
                       56.5 PERCENT
  WATER  MAKE  UP
                        OPEN  LOOP  1.04  GPM/MW
  SLUDGE  DISPOSAL
                       EXISTING FLY  ASH POND
  UNIT  COST
SEE APPENDIX A,  FGD SYSTEM ECONOMICS
  OPERATIONAL
   EXPERIENCE
 REFER TO THE BACKGROUND INFORMATION SECTION IN TABLE 3 OF THIS REPORT.
 THIS LIMESTONE SCRUBBING SYSTEM HAS PLACED IN SERVICE IN OCTOBER 1973.
 THE SCRUBBER PLANT CONSISTS OF TWO PARALLEL SCRUBBING TRAINS. PARTICU-
 LATE CONTROL IS PROVIDED BY TWO FLOODED-DISC SCRUBBERS. S02 CONTROL IS
 PROVIDED BY ONE PACKED (HUNTERS PACKING)  TOWER IA-SIDE). FLUE GAS CLEAN-
 ING WASTES ARE DISCHARGED TO AN EXISTING  FLY ASH POND. NO WATER IS RE-
 CYCLED BACK FROM THE DISPOSAL POND. IN-LINE STEAM REHEATERS RAISE THE
 GAS TEMPERATURE 40 F.
                                                24

-------
                                       BACKGROUND  INFORMATION
                                                 ON
                                            CHOLLA NO.  1

     THE CHOLLA POWER STATION, LOCATED NEAR JOSEPH CITY,  ARIZONA,  HAS  ONE  115-MW  COAL-FIRED  BOILER
IN SERVICE AND TWO 250-MW UNITS UNDER CONSTRUCTION.  CHOLLA  NO.  1  IS A  DRY-BOTTOM PULVERIZED-COAL-
FIREO UNIT DESIGNED BY COMBUSTION ENGINEERING.   THE  AVERAGE  CHARACTERISTICS  OF  THE COAL  BURNED  DUR-
ING THE COURSE OF 1975 ARE:  HEAT CONTENT OF  10,150  BTU/LB;  ASH  CONTENT  OF  13.45  PERCENT;  SULFUR
CONTENT OF 0.52 PERCENT; CHLORIDE OF 0.04 PERCENT  (MAX.);  AND MOISTURE  CONTENT  OF la.77  PERCENT.

     THE FGD SYSTEM AT THE CHOLLA PLANT WAS MANUFACTURED  BY  RESEARCH-COTTRELL,  AND INSTALLATION WAS
COMPLETED ON DECEMBER 3, 1973.  THE COMBINED  SULFUR  DIOXIDE  DESIGN REMOVAL  EFFICIENCY  (FOR BOTH
MODULES A AND B)  IS 58.5 PERCENT.  THE SYSTEM CONSISTS  OF  TWO PARALLEL  TRAINS  (MODULES  A  AND B).
EACH TRAIN IS DESIGNED FOR 240,000 ACFM THROUGHOUT AT 276  F, AND HANDLES APPROXIMATELY  50  PERCENT
OF THE BOILER'S FLUE GAS LOAD.  THE A-SIOE CONSISTS  OF  A  CEILCOTE-LINED  VARIABLE-THROAT  FLOODED
DISC SCRUBBER (FDS) FOLLOWED BY A PACKED TOWER  (MUNTER'S  PACKING). THE  B-SIDE  IS SIMILAR  IN DESIGN.
HOWEVER, THE TOWER IS NOT PACKED AND LIMESTONE  SLURRY IS  NOT CIRCULATED  THROUGH IT.  EITHER  ONE OH
BOTH OF THE SCRUBBERS CAN BE BY-PASSED.  GAS  LEAKAGE AROUND  EACH TRAIN  IS  ESTIMATED  TO  BE  ABOUT 4.5
PERCENT OF THE GAS BEING TREATED.  THE TOWER  PACKING, WHICH  IS APPROXIMATELY 2-FEET  THICK, IS CON-
STRUCTED OF POLYPROPYLENE CORRUGATED SHEETS JOINED TOGETHER  IN CRISS-CROSS  PATTERNS  SIMILAR  TO
HONEYCOMBS.  THE  TOWER MIST ELIMINATORS ARE CONSTRUCTED OF POLYPROPYLENE,  AND  THE REHEATERS  ARE
SHELL AND TUBE TYPE CONSISTING OF 3 STAINLESS STEEL  TUBE  BUNDLES PER UNIT.   THE STACK  IS  ACID
BRICK LINED.  PIPING AND RECIRCULATING PUMPS  ARE RUBBER LINED.

     LIMESTONE FOR THE FGO SYSTEM IS PURCHASED  IN  GROUND  FORM SUITABLE  FOR  SLURRYING.   THE MAIN
SOURCE OF SUPPLY  IS THE SUPERIOR CO.  LOCATED NEAR PHOENIX,  ARIZONA.   THIS  GRADE  OF  LIMESTONE IS
GENERALLY KNOWN AS RED WALL LIMESTONE AND IS  CONSIDERED A  VERY HIGH QUALITY  GRADE.  CHEMICAL SPEC-
IFICATIONS ARE:   MINIMUM CALCIUM OXIDE CONTENT,  52 PERCENT;  MINIMUM CALCIUM  CARBONATE  CONTENT,  95
PERCENT; MAXIMUM  MAGNESIUM OXIDE CONTENT, 2 PERCENT; MAXIMUM MAGNESIUM  CARBONATE  CONTENT,  0.5 PER-
CENT; MAXIMUM SILICA CONTENT,  1 PERCENT.

     THE PLANT HAS NO SLUDGE TREATMENT OR FIXATION SYSTEMS.  THE  SLUDGE  IS  PUMPED  TO  THE  FLY  ASH POND
ON AN  INTERMITTENT BASIS THROUGH A COMMON PIPING SYSTEM WITH THE FLY ASH.   NO  POND WATER  IS  RECYCLED
TO THE FGD SYSTEM (SOLAR EVAPORATION POND).   A  GENERAL  PROCESS FLOW DIAGRAM  OF  THE CHOLLA  FGD SYSTEM
IS PRESENTED  IN APPENDIX B.

PROBLMS  AND SOLUTIONS:  INITIAL AND SUBSEQUENT OPERATION

     DECEMBER,  1973 TO APRIL 2, 1974: BECAUSE OF A DIFFERENCE IN THE SIZE  OF THE  MAIN  DUCT AND  RE-
HEATER  TRANSITION DUCT, THE GAS FLOW PRODUCED HARMONIC  VIBRATIONS  IN THE REHEATER.  THE  VIBRATIONS
WERE PARTIALLY  DAMPED BY INSTALLATION OF BAFFLES.  ONE  OF  THE REHEATER  TUBE  BUNDLES  WAS  BADLY COR-
RODED  BY  ACID THAT CONDENSED  IN THE UNINSULATED DUCT UPSTREAM OF THE REHEATERS.  THE TUBE  BUNDLE WAS
REPLACED,  AND A BAFFLE WAS  INSTALLED TO DIVERT  CONDENSED  ACID FROM REHEATER  TUBES.  ALSO,  THE DUCT
UPSTREAM  OF THE REHEATEK WAS  INSULATED. THE ACID CONDENSATION OCCURED  ONLY  IN  THE 8-MOOULE WHICH
CONTAINS  NO  INTERNAL PACKING  AND THEREFORE HAS  A LOWER  DEGREE OF SULFUR  DIOXIDE REMOVAL
 (25  PERCENT).

     ANOTHER  PROBLEM RESULTED  BECAUSE OF SOLIDS BUILD UP  IN  THE  FDS STUFFING GLAND BOX  AND ON TOP
OF THE  SPRAY  DOME.  ALSO,  SOME LINES PLUGGED, PARTICULARLY WHEN  THE SYSTEM  OPERATED  AT  LOW FLOW
RATES.   SOLIDS  SETTLED  OUT  IN  STANDBY PUMPS,  AND EXCESSIVE FAN VIBRATIONS  OCCURRED BECAUSE OF ACCU-
MULATION  OF SCALE BUILDUP  WHEN THE UNIT WAS IDLt.  TO SOLVE  THESE  PROBLEMS,  THE PACKING  GLAND POSI-
TION WAS  REVERSED (INSTALLED  UPSIDE DOWN), THE  FAN WAS  SANDBLASTED, THE  PIPING  WAS MODIFIED  TO  ELIM-
 INATE  STAGNANT  POCKETS, AND PUMPS WERE FLUSHED  IMMEDIATELY AFTER REMOVAL FROM  SERVICE.

     OPERATION  OF THE SYSTEM  THROUGHOUT  1975  AND 1976 WAS  ACCOMPANIED  BY A  NUMBER OF MINOR PROBLEM
AREAS  INCLUDING:  SIGNIFICANT  CORROSION ATTACK IN THE VESSEL  WALLS  OF THE VENTURI  FLOODED-OISC
PARTICULATE SCRUBBER MODULE:  ACID CORROSION IN  THE B-SIDE  REHEATER HOUSING;  SCALE BUILDUP  IN THE
PIPEOUTLET  AT  THE SLUDGE/FLY  ASH EVAPORATION  POND; PLUGGING  IN THE SCRUBBER  TOWER PACKING  AND MIST
ELIMINATOR; EROSION  IN  THE  PUMPS; CORROSION IN  THE BOILER  EXHAUST  ELBOW  OF  THE  DUCTWORK  LEADING FROM
THE  SCRUBBERS  TO  THE STACK. ADDITIONAL INFORMATION AND  DATA  ON THE PERFORMANCE  OF THE  CHOLLA FGO
SYSTEM ARE  PROVIDED  IN  THE  TABLE THAT FOLLOWS.
                                                   25

-------
    ARIZONA PUBLIC SERVICE
MONTH

JAN. 74

FEB. 74
MAR. 74

APR. 74
MAY  74

JUN. 74
JUL. 74

AUG. 74
SEP. 74

OCT. 74
NOV. 74

DEC. 74
JAN. 75

FEB. 75
MAR. 75

APR. 75
MAY  75
 JUN. 75
JUL. 75
   RELIABILITY (X)
MODULE A     MODULE B
                                       FSD SYSTEM RELIABILITY
                                          CHOLLA UNIT NO. 1
                                                               CHOLLA UNIT NO.  1
                                                    COMMENTS
MAY  76
JUN. 76
JUL. 76
   97

  100
  100

   66
   98

  100
   97

   97
   95

   83
  100

  100
   98

   96
   88
   48
              100
              97
              76
              64
  100
 90

 94
 66

 57
 99

100
 92

 97
 99

 68
 98

100
 99

 99
 65
 40
                        100
                         98
AUG.
SEP.
OCT.
NOV.
DEC.
JAN.
FEB.
MAR.
APR.
75
75
75
75
75
76
76
76
76
95
96
84
100
100
99


99
100
97
55
80
100
99


98
                        100
                         39
                         98
 ANNUAL BOILER AND FGD SYSTEM OVERHAUL.
MODULES WERE BOTH OFF-LINE FOR MOST OF MONTH FOR SCHEDULED RE-
PAIRS AND CLEANING.

PLUGGING IN THE A-SIDE ABSORBER PACKING AND MIST ELININATORS WAS
OBSERVED.  NO OTHER MAJOR PROBLEMS MERE ENCOUNTERED DURING
THE PERIOD.
MODULES WERE SHUT DOWN TO CLEAN FLOW RESTRICTIONS IN FLOODED-
DISC RECIRCULATION LINES.

THE A SIDE WAS SHUT DOWN ONCE FOR INSPECTION.
MINOR OUTAGE RESULTED FROM PLUGGED FDS RECIRCULATION LINES.

OUTAGES RESULTED FROM SCHEDULED EQUIPMENT OVERHAULS AND RECOAT-
ING OF VESSELS.
NO MAJOR OUTAGES OR PROBLEMS OCCURED DURING THE REPORT PERIOD.

MINOR PROBLEMS ENCOUNTERED INCLUDED RECYCLE PUMP REBUILDING AND
MALFUNCTIONING OF THE B-SIDE REHEATER COIL.
MODULE A OPERATED 715 HOURS DURING THE REPORT MONTH, AND MODULE
B OPERATED 654 HOURS.  MODULE A EXPERIENCED SOME MINOR VALVE
AND LINE PLUGGING.  MODULE B OPERATING HOURS WERE LOWER BECAUSE
OF REDUCED SYSTEM REQUIREMENTS.
            THE UNIT IS CURRENTLY EXPERIENCING COATING FAILURES IN THE
            ELBOW OF THE SCRUBBER EXHAUST DUCT.  ALSO, THE UTILITY PERFORM-
            ED SOME MINOR REPAIRS TO THE HOUSING OF THE B-SIDE REHEATER.

            DURING THE MONTH THE A-SIDE EXPERIENCED SOME CORROSION AND
            PLUGGING PROBLEMS IN THE REHEATER TUBES.  IN ADDITION TO PLUGGED
            FOS LINES, PACKING AND MIST ELIMINATORS, APS ALSO REPORTED THAT
            HEAVY PUMP MAINTENANCE WAS REQUIRED.

            LOW RELIABILITY FACTORS FOR THE MONTH OF JUNE RESULTED FROM A
            SCHEDULED MID-YEAR SCRUBBER SHUTDOWN FOR MAINTENANCE, INSPEC-
            TION AND REPAIRS.  SOME SCALING AND CORROSION PROBLEMS WERE
            UNCOVERED IN THE SYSTEM'S RECYCLE TANKS.

            DURING THE JULY-AUGUST PERIOD THE UTILITY REPORTED THAT REPAIRS
                                                  26

-------
    ARIZONA PUBLIC SERVICE

              RELIABILITY   UJ
MONTH      MODULE A     MODULE  B
AUG. 76      100        100
                          FGD  SYSTEM  RELIABILITY
                            CHOLLA UNIT  NO.  i
                                                  CHOLLA UNIT NO.  1
SEP. 76
OCT. 76
NOV. 76
DEC.  76
              100
              56
               96
               96
                         100
                          56
                          98
                         100
                                                   COMMENTS
                       TO  THE  COATING  IN  THE  ELBOW  OF  THE SCRUBBER EXHAUST  OUCT  WERE
                       COMPLETED.   A MALFUNCTIONING SOLENOID  VALVE IN THE  MIST  ELIM-
                       INATOR  WASH  SYSTEM OF  THE  B-SIDE,  PREVENTING ADEQUATE  WASHING,
                       RESULTED  IN  A MINOR SCRUBBER OUTAGE.


                       THE  BQILER REMAINED IN SERVICE  THE ENTIRE  MONTH.   A-SIDE  SERVICE
                       TIME  WAS  720 HOURS. B-SIDE  SERVICE TIME  WAS 676  HOURS.   NO
                       SIGNIFICANT  PROBLEMS WERE  REPORTED.


                       THE  BOILER WAS  IN  SERVICE  417 HOURS DURING THE MONTH.   A-SIDE
                       AND  B-SIDE OPERATIONAL HOURS WERE  115  AND  277  RESPECTIVELY.


                       DURING  THE MONTH THE BOILER, A-SIDE AND B-SIDE TRAINS  WERE  IN
                       SERVICE 720, 682 AND 556 HOURS,  RESPECTIVELY.   TWO  MINOR  FORCED
                       SCRUBBER  OUTAGES OCCURRED  DURING THE PERIOD DUE TO  A HEHEATER
                       STEAM LEAK AND  INLET GAS DAMPER  ADJUSTMENTS TO BOTH  THE  A-SIOE
                       AND  B-SIDE SCRUBBING TRAINS.


                       BOILER, A-SIDE,  AND B-SIDE OPERATION HOURS FOR THE  MONTH  WERE
                       744,  742  AND 498 HOURS, RESPECTIVELY.  ONE OUTAGE  WAS  REPORTED
                       BECAUSE OF AN ADDITIONAL ADJUSTMENT TO THE A-SIDE  GAS  INLET
                       DAMPER.
 NOTE:  THE  PERFORMANCE  INDEX  VALUES  CONTAINED  IN  THE  TEXT  OF  THIS  TABLE  ARE  BASED  UPON  THE  MODULES'
 ACTUAL SERVICE  TIME  FOR  THE  PERIOD  VERSUS  THE NUMBER OF  HOURS  THE  MODULES  ARE  CALLED UPON  TO  OPER-
 ATE  FOR THE  SAME  PERIOD.  THE MODULES  OPERATE  ON  A  DEMAND-ONLY  BASIS.  FLUE  GAS  IS  BYPASSED  AROUND  THE
 MODULES WHEN THEY ARE  NOT REQUIRED  FOR  SERVICE.
 JAN.  77



 FEB.  77
 72



 99
 93



 99
 MAR.  77



 APR.  77


 MAY.  77
 72



100

 87
 93



100

 87
 JUN. 77
 JUL. 77
 AUG. 77



 SEP. 77





 OCT. 77
100
 97
 97



100





100
100
 99
 99



100





100
SERVICE HOURS FOR JANUARY:  BOILER = 744,  A-SIDE = 532,  B-SIDE *
684.

SERVICE HOURS FOR FEBRUARYS BOILER = 672,  A-SIDE s fe4B, B-SIDt =
591.  THE MUNTERS PACKING IN THE A-SIDE TOWER WAS REPLACED.   IN
ADDITION SOME MINOR PROBLEMS WERE ENCOUNTERED IN THE FORM OF
SCRUBBER VESSEL PLUGGING, MINOR CORROSION  AND LIQUID PIPING
PROBLEMS, AND MECHANICAL DIFFICULTIES WITH THE BY-PASS  DAMPERS.
AVERAGE S02 INLET/OUTLET VALVES DURING THE PERIOD WERE  350 PPM
AND 175 PPM.

SERVICE HOURS FOR MARCH: BOILER = 744, A-SIDE = 532, B-SIDE  =
684.

SERVICE HOURS FOR APRIL: BOILER = 638, A-SIDE = 635, B-SIDE  =
629.
SERVICE HOURS FOR MAY:  BOILER s 645, A-SIDE = 645, B-SIDE =  645.
OUTAGE TIME FOR THE BOILER  AND THE FGD SYSTEM WERE A RESULT  OF
THE SCHEDULED MID-YEAR  SCRUBBER CLEANOUT.   DURING MAY,  RE-
SEARCH-COTTRELL PERSONNEL CONDUCTED FORCED OXIDATION TESTS,  BY
BLOWING AIR INTO THE FLOODED DISC SCRUBBER AND CONVERTING ALL
CAS03 TO CAS04 FOR SUPERIOR SLUDGE OEWATERING, HANDLING AND
SCALE-FREE OPERATION.

SERVICE HOURS FOR JUNE: BOILER, A-SIDE AND B-SIDE = 720.
SERVICE HOURS FOR JULY: BOILER = 744, A-SIDE = 724, B-SIDE =
734.  MINOR PROBLEMS INCLUDED A LEAK IN THE LIMESTONE SLURRY
TANK AND A LEAK IN THE  B-SIDE RETURN LIME  FROM THE FDS  TO THE
FDS TANK.  RESEARCH-COTTRELL PERSONNEL ARE STILL ON THE PLANT
SITE, CONTINUING FORCED OXIDATION STUDIES.

SERVICE HOURS FOR AUGUST: BOILER = 744, A-SIDE = 723.3, B-SIDE :
733.7.

FOR SEPTEMBER: BOILER = 720, A-SIDE a 717.9, B-SIDE = 717.8.
THE DOWNTIME WAS REQUIRED TO REPAIR TWO DIFFERENT LEAKS.  ONE
LEAK OCCURRED AT THE SLURRY DISPOSAL TANK.  THE OTHER WAS
LOCATED IN THE FDS RETURN LINE BETWEEN THE TOWER AND FDS TANK.

SERVICE HOURS FOR OCTOBER:  BOILER * 744,  A-SIDE AND B-SIDE
743.2.  OPERATIONS WERE VERY SUCCESSFUL IN OCTOBER  1977.
                                                   27

-------
ARIZONA PUBLIC SERVICE            FGD SYSTEM RELIABILITY            CHOLLA UNIT NO. 1
                                          CHOLLA UNIT NU. 1
              RELIABILITY U)
MONTH      MODULE A     MODULE B                                COMMENTS

NOV. 77      100         98         SERVICE HOURS FOR NOVEMBER!  BOILER AND A-SIDE = 166.5/ B-SIDE s
                                    1*12.  B-SIDE OUTAGE DUE  TO LEAKS IN VENTURI SECTION Of SCRUBBER
                                    AND EXPANSION JOINT IN RECYCLE PUMP.  BOILER OPERATED ONLY 168.5
                                    HOURS BECAUSE OF A SHUTDOWN  FOR OVERHAUL IN LAST HALF OF NOVEM-
                                    BER.  SCHEDULED START-UP IS  MID-DECEMBER.

DEC. 77                             THE BOILER AND THE SCRUBBERS WERE DOWN AS  THE OVERHAUL PERIOD
                                    CONTINUED.  THIS WAS A MAJOR OVERHAUL AND  EXTENDED INTO JAN.  78.
JAN. 78       97         91        DURING THE OVERHAUL THE FLOODED DISC SCRUBBER TANK HEADER FOR
                                    SLURRY LIME WAS DAMAGED  REPAIRED.  THE BOILER WAS OPERATED
                                    ONLY 135 HRS. DURING JANUARY AS THE OVERHAUL HAD EXTENDED INTO
                                    THIS MONTH.
                                                  28

-------
                  TABLE 3
PERFORMANCE DESCRIPTION FOR OPERATIONAL FGD  SYSTEMS  THROUGH   01/78
 UTILITY NAME

 UNIT NAME

 UNIT LOCATION

 UNIT RATING

 FUEL CHARACTERISTICS

 FGO VENDOR

 PROCESS

 NEW OR RETROFIT

 START UP DATE

 FGD STATUS

 EFFICIENCY,
   PARTICULATES
 COLUMBUS  &  SOUTHERN OHIO ELEC,

 CONESVILLE  NO 5

 CONESVILLE  OHIO

  400  MM

 COAL  4.5  -  4.9 PERCENT SULFUR

 UNIVERSAL OIL PRODUCTS

 LIME  SCRUBBING

 NEW

  1/77

 OPERATIONAL


 99.6  PERCENT
   soe
                        89.5  PERCENT
  WATER MAKE UP
                        OPEN LOOP
  SLUDGE DISPOSAL
 PUMPED TO A LANDFILL
  UNIT COST
SEE APPENDIX A, FGD SYSTEM ECONOMICS
  OPERATIONAL
   EXPERIENCE
 REFER TO THE BACKGROUND INFORMATION SECTION IN TABLE 3 OF THIS REPORT.
 THE BOILER AND ESP WERE COMPLETED AND PLACED IN SERVICE IN SEPT.  1976.
 THE B-SIOE MODULE BECAME AVAILABLE FOR SERVICE IN JANUARY 1977.
 COMMERCIAL OPERATIONS WERE ACHIEVED ON FEBRUARY 13,  1977. THE EMISSION
 CONTROL SYSTEM FOR THIS UNIT CONSISTS OF A COLD-SIDE ESP FOLLOWED BY
 TWO TCA LIME SCRUBBING MODULES SUPPLIED BY UOP. DRAVO IS SUPPLYING THE
 THIOSORBIC LIME SCRUBBING REAGENT. IUCS IS SUPPLYING THEIR POZ-0-TEC
 SLUDGE STABILAZATION FACILITY.
                                                29

-------
                                       BACKGROUND INFORMATION
                                                 ON
                                          CONESVILLE NO. 5

     THE CONESVILLE POWER STATION IS LOCATED ON THE MUSKINGUM RIVER, APPROXIMATELY 740 FEET  ABOVE
SEA LEVELr NEAR COSHOCTON, IN NORTHEAST OHIO.  THE PLANT HAS A CURRENT CAPACITY OF 1644 MW  (NAME-
PLATE)  WITH AN ADDITIONAL 111 MW UNDER CONSTRUCTION.  UNITS 1,2, AND 3 HAVE A COMBINED CAPACITY  OF
433 MW (UNITS 1 AND 2 HAVE A COMMON STACK).  UNIT NO.4 IS RATED AT 800 MW AND UNIT NO.5 IS  RATED AT
411 MW.  UNIT NO.6, CURRENTLY UNDER CONSTRUCTION WILL ALSO BE RATED AT 411 MW.  UNITS 3 AND  4  HAVE
SEPARATE STACKS.  UNITS 5 AND 6 SHARE A COMMON STACK,

     BOILER NO. 5 IS A DRY-BOTTOM, PULVERIZED-COAL-FIRED COMBUSTION ENGINEERING UNIT, INSTALLED  IN
1976.  THE BOILER IS FIRED WITH 25 PERCENT EXCESS AIR AND IS RATED AT 89 PERCENT EFFICIENCY.   THE
HEAT RATE IS 8600 BTU/KWH.  THE PLANT BURNS A MIXTURE OF HIGH-SULFUR OHIO COAL, WITH SULFUR  CONTENTS
OF FROM 4.2 TO 5.1 PERCENT, ASH CONTENTS OF FROM 12 TO 19 PERCENT, AND HEATING VALUES OF FROM  10,300
TO 11,220 BTU/LB.  FORTY PERCENT OF THE COAL FIRED COMES BY CONVEYOR FROM A NEARBY (7 MILES  DISTANT)
COAL MINE COMPLEX.  THE REMAINDER IS TRUCKED IN FROM SOUTHEAST OHIO.

     THE AIR POLLUTION CONTROL SYSTEM AT CONESVILLE NO. 5 CONSISTS OF A RESEARCH-COTTRELL COLO-SIDE
ESP, FOLLOWED BY TWO UNIVERSAL OIL PRODUCTS (UOP) 302 ABSORBER MODULES.  THE ESP IS DESIGNED FOR
99.65 PERCENT REMOVAL EFFICIENCY AND THE TURBULENT CONTACT ABSORBERS (TCA) MODULES ARE DESIGNED  FOH
S02 REMOVAL EFFICIENCY OF 89.6 PERCENT.  THE SYSTEM IS DESIGNED FOR AN OUTLET S02 LOADING OF 1.0
LB/MILLION BTU INPUT.  BOILER I.D. FANS ARE LOCATED IMMEDIATELY DOWNSTREAM OF THE ESP.

     FOLLOWING THE I.D. FANS, THE FLUE GAS IS HEADERED INTO THE TWO PARALLEL TCA SCRUBBING  TRAINS,
EACH ABSORBER CAPABLE OF HANDLING 60 PERCENT OF THE FLUE GAS FLOW.  A PRESATURATOR SECTION,  CONSTR-
UCTED OF CARPENTER 20, QUENCHES THE HOT GAS, LOWERING THE TEMPERATURE FROM 286F TO 125F, AND PROVID-
ING INITIAL S02 REMOVAL.  THE GAS THEN ENTERS THE NEOPRENE-LINED,  CARBON STEEL ABSORBER MODULES,
WHERE TWO LEVELS OF 1.5 INCH BALLS PROVIDE TURBULENT BEDS FOR FINAL S02 REMOVAL.  THE LOWER  STAGE IS
COMPARTMENTED TO MAINTAIN UNIFORM BALL DEPTH.  FOLLOWING EACH ABSORBER MODULE, THE FLUE GAS  PASSES
THROUGH A FIBERGLASS TRAP-OUT TRAY AND TWO HORIZONTAL BANKS OF CHEVRON-TYPE MIST ELIMINATORS.  THE
BOTTOM OF THE TRAP-OUT TRAY IS WASHED INTERMITTENTLY AND THE LOWER MIST ELIMINATOR IS WASHED CONTIN-
UALLY WITH RECYCLED POND WATER.  THE FLUE GAS FROM THE PARALLEL ABSORBER TRAINS IS THEN HEAOERED
INTO THE 800-FT, CEILCOTE-LINEO STACK.  FOLLOWING THE BOILER I.D.  FAN THERE IS BYPASS BREECHING
AROUND THE ENTIRE SCRUBBER LOOP.  THERE IS NO STACK GAS REHEAT CURRENTLY BEING EMPLOYED, ALTHOUGH
THE POSSIBILITY EXISTS OF ADD-ON REHEAT AT SOME FUTURE DATE.

     DRAVO THIOSORBIC LIME FROM MAYSVILLE, KENTUCKY IS UTILIZED IN THE UOP SCRUBBER MODULES  AT A
STOICHIOMETRIC RATIO OF 1.1.  THE CALCINED, PELLETIZED LIME HAS A  NOMINAL PARTICLE DIAMETER  OF 1.75
INCH, AN MGO CONTENT OF 3 TO 8 PERCENT AND A CAO CONTENT OF 90 TO  95 PERCENT.  THE LIME SLAKER DISC-
HARGED THE 20 PERCENT SOLIDS SLURRY INTO AN AGITATED LIME SLURRY SUMP WHERE IT IS RETAINED FOR A
5-MINUTE PERIOD PRIOR TO TRANSFER TO THE LIME SLURRY STORAGE TANK, WHICH HANDLES THE SURGE REQUIRE-
MENTS OF THE ABSORPTION SYSTEM.  THE TRANSFER OF SLURRY FROM THE STORAGE TANK TO THE TCA RECYCLE
TANKS IS ACCOMPLISHED BY VARIABLE SPEED PUMPS WHICH RESPOND TO CHANGING S02 AND LOAD CONDITIONS  VIA
A  PH MONITOR.  THE SCRUBBING LIQUOR CONTAINS 7 TO 12 PERCENT SOLIDS.  THE ABSORBENT LIQUOR  IS  RECIR-
CULATED BY 4 PUMPS d STANDBY) EACH RATED AT 12,000 GPM.  SCRUBBER OUTLET PH is 5.8, AND PH  IN THE
RECYCLE TANK IS APPROXIMATELY 6.8.

     A BLEED STREAM OF SPENT REACTION PRODUCTS IS CONTINUOUSLY WITHDRAWN FROM THE TANK PUMPED  TO THE
THICKENER SYSTEM.  THE THICKENER IS 100 FT IN DIAMETER AND 14 FT DEEP IN THE CENTER.  HERE THE RE-
ACTION PRODUCT SLURRY IS CONCENTRATED TO AN UNDERFLOW COMPOSITION  OF APPROXIMATELY 30-35 PERCENT
SOLIDS.  THIS UNDERFLOW IS CYCLED TO THE IUCS FIXATION FACILITIES  WHERE IT IS FURTHER THICKENED,
VACUUM FILTERED AND MIXED WITH A BLEND OF DRY FLY ASH AND LIME TO  FORM A 73 PERCENT SOLIDS SUBSTANCE
(IUCS POZ-0-TEC). THE PRODUCT IS BEING CYCLED TO A DIKED POND.

     THE WASTE WATER POND, WHICH WILL RECEIVE THE ASH WATER, COOLING WATER SLOWDOWN AND WATER  FROM
THE SLUDGE TREATMENT PLANT, IS EXPECTED TO OVERFLOW INTO THE MUSKINGUM RIVER DURING ALL PLANT  OPER-
ATING PERIODS (LOW AND HIGH LOAD OPERATIONS).  THEREFORE, ALL SYSTEM OPERATIONS WILL BE CONDUCTED IN
A  WATER POSITIVE MODE.

     REFER TO APPENDIX B FOR A GENERAL PROCESS FLOW DIAGRAM.  THE  OPERATING HISTORY OF THE
CONESVILLE UNIT IS SUMMARIZED CHRONOLOGICALLY IN THE PERFORMANCE TABLE THAT FOLLOWS.
                                                  30

-------
COLUMBUS & SOUTHERN OHIO ELECTRIC
OPERATING HISTORY
  CONESVILLE NO. 5
                                                                 CONESVILLE UNIT.  5
               MODULE          MODULE
             AVAILABILITY    OPERABILITY
             (PERCENT)       (PERCENT)
MONTH/YR    A        B        A       8
DEC. 76
 JAN.  77
 FEB.  77
                                     43
                             COMMENTS
    S02 REMOVAL OPERATIONS WERE SCHEDULED TO COMMENCE IN
    DECEMBER.  HOWEVER A MAJOR FIRE IN MODULE NO. SA DELAYED
    START-UP.  THE FIRE CAUSED $2.1 MILLION DAMAGE TO THE
    MODULE.  THE UTILITY'S INSURANCE COVERED THE DAMAGE AND
    A NErt SCRUBBER MODULE WILL BE PURCHASED FROM AND IN-
    STALLED BY U.O.P.  THE 5A MODULE IS SCHEDULED TO COM-
    MENCE OPERATIONS IN NOVEMBER 1977.
    THE UTILITY IS CURRENTLY CONDUCTING AIR AND WATER TESTS
    ON MODULE 56 AND SCRUBBING OPERATIONS WITH 58 ARE NOW
    SCHEDULED FOR JANUARY.

    INITIAL START-UP FOR DEBUGGING AND COMMISSIONING PUR-
    POSES OCCURRED IN EARLY JANUARY.  EARLY OPERATIONS WERE
    MARKED BY COLD WEATHER RELATED PROBLEMS SUCH AS FROZEN
    LINES AND GEARS, CRACKED FLANGES, A FROZEN LIME BELT
    CONVEYOR, AND A FROZEN PIPELINE FROM THE THICKENER TO
    THE IUCS FACILITY.  COMMERCIAL AVAILABILITY FOR SERVICE
    OCCURRED ON JANUARY 27.  NO JANUARY OPERATING HOURS ARE
    AVAILABLE.

    COMMERCIAL START-UP OF MODULE 5B ACHIEVED ON FEBRUARY
    13, 1977.  AFTER START-UP, THE SCRUBBER LOGGED 286 HOURS
    OF OPERATION.  THE LONGEST PERIOD OF CONTINUOUS OPERA-
    TION WAS 132 HOURS.  THE BOILER LOGGED 668 HOURS DURING
    FEBRUARY.  PRUBLEMS INCLUDED PRESSURE SURGES IN THE
    PRESATURATOR PIPING LINE, UNSATISFACTORY OPERATION OF
    THE CONTINUOUS 502 ANALYZERS, POOR VELOCITY DISTRIBUTION
    THROUGH THE TCA BEDS, AND CARRYOVER OF SCRUBBING LIQUID
    INTO THE MIST ELIMINATOR SECTION.  THE ESP IS REPORTED
    TO BE OPERATING SATISFACTORILY.  COMPLIANCE TESTING FOR
    THIS UNIT IS SCHEDULED FOR MAY 1977.
                                                   31

-------
COLUMBUS & SOUTHERN OHIO ELECTRIC
                                  CONESVILLE UNIT NO. 5
           OPERATION TIME (HR)
PERIOD   BOILER    A-SIOE    B-SIDE
APR. 77    665                361
AVAILABILITY = 40 PERCENT
OPERABILITY = 38 PERCENT
RELIABILITY = 39 PERCENT
UTILIZATION = 36 PERCENT
MAY 77     712
AVAILABILITY = SB PERCENT
OPERABILITY a 50 PERCENT
RELIABILITY = 51 PERCENT
UTILIZATION = 48 PERCENT
JUN. 77    713
AVAILABILITY » 66 PERCENT
OPERABILITY a 59 PERCENT
RELIABILITY = 60 PERCENT
UTILIZATION a 58 PERCENT
355
418
 JUL. 77
           744
 AUG.  77                U
 ALL  INDEX  VALUES = 0 PERCENT
 SEP-  77     469
 AVAILABILITY  = 52.9 PERCENT
 PEPRABILITY = 39.9 PERCENT
 RELIABILITY » 46.9 PERCENT
 UTILIZATION x 26 PERCENT

 OCT.  77     559         0
 AVAILABILITY  (X) =
 OPERABILITY (X) =
 RELIABILITY (X) s
 UTILIZATION (X) «

 NOV.  77     715         9
 AVAILABILITY  (X) a    10
 OPERABILITY (X) s      n
 RELIABILITY (X) s      4
 UTILIZATION (X) a1      4
DEC. 77              162
AVAILABILITY  (X) a    93
OPERABILITY  (X) a     64
RELIABILITY  (X) a     62
UTILIZATION  CX) =    22
                              187
135
 32
 24
 25
 16

234
 33
 33
 33
 33
199
 97
 79
 76
 27
                         COMMENTS
THE UTILITY REPORTED A NUMBER OF PROBLEM AREAS REGARDING
SCRUBBER OPERATIONS DURING THE REPORT PERIOD.  SPECIF-
ICALLY, SOME CORROSION HAS BEEN REPORTED IN THE PRESAT-
URATOR AREA (316 SS CONSTRUCTION), THE RUBBER LINER  IN
THE RECYCLE TANK IS PEELING OFF (PROBABLY AN APPLICATION
PROBLEM), SOME PLUGGING IN THE TUBE THICKENERS HAS OC-
CURRED, AND THE QUALITY OF THE LIME SLURRY HAS BEEN  A
REAL PROBLEM AREA (ROCKS UP TO FIVE INCHES IN DIAMETER
HAVE BEEN DETECTED).  THE LATTER ITEM HAS PROMPTED
DRAVO TO INSTALL MECHANICAL SEPARATORS AND METAL DETEC-
TORS AT THE LIME SHIPMENT FACILITY,  A STACK OUTLET
TEMPERATURE OF 200 F IS BEING MAINTAINED IN ORDER TO
MINIMIZE ACID RAINOUT AND STACK CORROSION PROBLEMS.
THE B-SIDE MODULE DID NOT OPERATE THE ENTIRE MONTH
PENDING COMPLETION OF A NUMBER OF NECESSARY MODIFICA-
TIONS AND REPAIRS.  THE MAJOR ITEMS ADDRESSED DURING
THE PERIOD INCLUDED:
    *M MODIFICATIONS TO THE UNIT PROCESS CONTROL SYSTEM
     AND INSTRUMENTATION LOOPS.
    *REPAIRS TO THE RECLAIM WATER PIPING NETWORK.
    •REPAIRS TO THE ABSORBER LINER.
    •REPAIRS TO THE PIPING BETWEEN THE THICKENER AND
     IUCS BUILDING.
THE UTILITY IS CURRENTLY PLANNING TO CONDUCT A PARTICU-
LATE DROP TEST DURING THE MONTH OF SEPTEMBER.
THE REPLACEMENT A-SIOE TCA MODULE REPLACING THE ORIGINAL
MODULE DESTROYED BY FIRE DECEMBER OF 1976 IS EXPECTED
TO BE AVAILABLE FOR COMMERCIAL SERVICE IN JANUARY 1978.
THE SCRUBBER WAS NOT OPERATING THE ENTIRE MONTH.  RE-
PAIRS AND MODIFICATIONS CONTINUED UNTIL SEPTEMBER 13.
THERE WERE SOME WEATHER-RELATED DELAYS.
THERE HAD BEEN NO PROBLEMS RECORDED SINCE THE SCRUBBER
OPERATION BEGAN AGAIN ON SEPTEMBER 13.
THE UTILITY IS PREPARING FOR AN S02 AND PARTICULATE DROP
TEST PUSHED BACK FROM SEPTEMBER, AS PREVIOUSLY REPORTED,
TO THE WEEK OF OCTOBER 24.
B-MODULE HAD TO BE RELINED IN SOME AREAS WITH NEOPRENE
RUBBER.  SCRUBBER WAS DOWN FROM OCT. 10 TO NOV. 10.
MODULE A WENT BACK ON LINE NOV. 21.  DURING LOW LOAD
PERIODS SOLIDS BUILD UP TENDED TO CAUSE PLUGGING BECAUSE
OF LOW FLOW RATES.  DURING LOW LOAD PERIODS ALL GAS WAS
DUCTED THROUGH ONE SCRUBBER WHILE THE OTHER WAS SHUT-
DOWN.
DURING THE DECEMBER 1977 TO MARCH 1978 SHUTDOWN, THE
CARBON STEEL FLUE WILL BE REPLACED BY ACID-bRICK LINED
STACK.

CONESVILLE NO. 5 WENT DOWN DECEMBER 12 FOR A 3-MONTH
SCHEDULED OUTAGE.  MODULE A WAS STARTED DECEMBER 3 AND
OPERATED AS MUCH AS POSSIBLE THROUGH DECEMBER 12.  MOD-
ULE B OPERATED DECEMBER 1 THROUGH 12.  THE UNIT WENT
DOWN FOR A COMPLETE OVERHAUL TO CHECK HOW WELL VENDOR
SPECS WERE ACHIEVED ON THE BOILER AND TURBINES.  THE
UNIT IS SCHEDULED TO BE BACK ON LINE IN MID-MARCH BUT
THIS MAY BE PUSHED BACK TO APRIL 1ST.  RELINING OF THE
STACK IS STILL CONTINUING
JAN. 78               00
ALL INDEX VALUES = 0 PERCENT
                                                  32

-------
                  TABLE 3
PERFORMANCE DESCRIPTION FOR OPERATIONAL F60 SYSTEMS  THROUGH   01/78
 UTILITY NAME

 UNIT NAME

 UNIT LOCATION

 UNIT RATING
 DUOUESNE  LIGHT

 ELRAMA  POWER  STATION

 ELRAMA  PENNSYLVANIA

  510  MM
 FUEL CHARACTERISTICS  COAL   1.0  -  2.8  PERCENT  SULFUR
 FGD VENDOR

 PROCESS

 NEW OR RETROFIT

 START UP DATE

 FGD STATUS

 EFFICIENCYr
   PARTICULATES
 CHEMICO

 LIME  SCRUBBING

 RETROFIT

 10/75

 OPERATIONAL


 99 PERCENT
   802
                        83  PERCENT  DESIGN  -  2X  S  COAL
  WATER  MAKE  UP
 OPEN LOOP
  SLUDGE  DISPOSAL
 HAULAWAY TO OFF SITE LANDFILL
  UNIT COST
SEE APPENDIX A,  FGD SYSTEM ECONOMICS
  OPERATIONAL
   EXPERIENCE
 REFER TO THE BACKGROUND INFORMATION SECTION  IN  TABLE  3  OF  THIS  REPORT.
 OPERATIONS ARE CONTINUING WITH THREE BOILERS COUPLED  INTO  THE FIVE-MODULE
 SCRUBBING SYSTEM.  THE PLANT IS FIRING  1.0 - 2.8  PERCENT SULFUR COAL.
 SCRUBBING WASTES ARE CHEMICALLY FIXATED BY THE  IUCS  SYSTEM AND  LANDFILL-
 ED.
                                                33

-------
                                       BACKGROUND INFORMATION
                                                 ON
                                       EIRAMA POWER STATION

     DUOUENSE LIGHT COMPANY, AN INVESTOR-OWNED ELECTRIC UTILITY, SERVES ABOUT ONE-HALF CUSTOMERS  IN
SOUTHWESTERN PENNSYLVANIA AND HAS A NET GENERATING CAPABILITY OF APPROXIMATELY 2500 MW.  THIS CAP-
ABILITY IS GENERATED BY COMBUSTION TURBINES IN SIMPLE AND COMBINED-CYCLE MOOES, BY NUCLEAR PLANTS,
AND BY COAL-FIRED POWER STATIONS.  THE COMPANY IS SOLE OWNER AND OPERATOR OF THREE COAL-FIRED
STATIONS, TWO OF WHICH HAVE BEEN RETROFITTED WITH WET SCRUBBERS USING LIME AS THE ABSORBING
REAGENT.

     THE SCRUBBER FACILITY AT THE 494-MW ELRAMA STATION IS ALMOST IDENTICAL TO THE SYSTEM AT THE
PHILLIPS STATION.  GIBB & HILL WAS THE A-E FIRM AND CHEMICO SCRUBBERS HAVE BEEN INSTALLED WITHIN
THE SAME DESIGNATED BATTERY LIMITS AS PHILLIPS.  MECHANICAL AND ELECTRICAL DUST-REMOVAL EQUIPMENT
REMOVES MOST PARTICULATES FROM THE BOILER EMISSIONS, AND THE GAS TO AND FROM THE SCRUBBERS IS
HEADERED IN THE SAME WAY.  UNLIKE THE PHILLIPS SYSTEM, HOWEVER, THERE ARE FOUR BOILERS, EACH WITH
ITS OWN TURBINE GENERATOR.  FIVE SINGLE-STAGE SCRUBBERS WERE INSTALLED, WITH THE INTENTION THAT
KNOWLEDGE GAINED FROM THE TEST PROGRAM AT PHILLIPS WOULD BE APPLIED TO ELRAMA TO ENABLE COMPLIANCE
WITH EMISSION REGULATIONS (0.6 LB. S02/MILLION BTU).

     THE FIRST ELRAMA SCRUBBER WAS PLACED IN SERVICE ON OCTOBER 26, 1975.  IT HAD BEEN SCHEDULED FOR
AN EARLIER STARTUP DATE, BUT BECAUSE OF THE SEVERITY AND NUMBER OF PROBLEMS ENCOUNTERED AT PHILLIPS,
STARTUP WAS DELAYED UNTIL MANY OF THE PROBLEMS AT PHILLIPS WERE RESOLVED AND THE MODIFICATIONS COULD
BE INCORPORATED AT BOTH STATIONS.

     THE SCRUBBERS ARE 30 FT DIA X 60 FT HIGH AND LINED WITH CEILCOTE.  THE GAS FLOW RATE IS 550,000
ACFM AT 325 F.  THE OUTLET GAS TEMPERATURE IS 120 F.  THE LIQUID RECIRCULATION RATE IS 16,000 GPM
AND THE SLURRY CONTAINS 3-5X SOLIDS.  A PH OF 6 IS MAINTAINED IN THE SCRUBBER.  THE I.D. FANS ARE
RUBBER LINED AND HAVE ssoo HP.  THE OVERALL PRESSURE DROP is ABOUT 30 IN WG.  THE RECIRCULATING
PUMPS  ARE 317 L SS,  WHEREAS THE INTERCONNECTING PIPING IS RUBBER LINED.

     BOILER NO. 2 WAS INITIALLY CONNECTED TO THE FGD SYSTEM ON OCTOBER 26, 1975.  THIS BOILER HAS AN
EQUIVALENT CAPACITY OF APPROXIMATELY 100 MW, AND THE EMISSIONS ARE HANDLED BY ONE SCRUBBER.  TO
ENSURE RELIABILITY IN THE CASE OF A SCRUBBER MALFUNCTION, TWO SCRUBBERS ARE OPERATED AT PARTIAL LOAD
TO PROTECT THE BOILER AND TURBINE GENERATOR AGAINST A TRIP-OFF.

     THE BOILER OPERATED CONTINUOUSLY ON THE SCRUBBER SYSTEM THROUGH JANUARY 1976.  TWO MINOR
OUTAGES OCCURRED DURING THIS PERIOD, ONE CAUSED BY INOPERATIVE THROAT DAMPERS AND THE OTHER
INVOLVING FAILURE OF A LIME FEEDER BELT.  ON FEB. n, 197&, A SECOND BOILER WAS COUPLED INTO THE
SCRUBBER COMPLEX.  PRESENTLY, 2 UNITS ARE THE MAXIMUM THAT CAN BE TIED INTO THE SCRUBBER PLANT.  TO
DATE,  THE UTILITY HAS ENCOUNTERED THE USUAL MINOR STARTUP PROBLEMS AND SOME MAJOR PROBLEMS AS WELL.
THE MAJOR PROBLEMS HAVE BEEN FROZEN PIPES AND THICKENERS, THE LATTER INVOLVING HARDWARE AND DESIGN
ASSOCIATED WITH RECIRCULATION OF THE SLUDGE WITHIN THE THICKENERS TO ATTAIN 30 TO 40 PERCENT SOLIDS
CONCENTRATION.

     THE SLUDGE BEING GENERATED AT THIS STATION IS TREATED BY THE IUCS METHOD, WHICH EMPLOYS A
VACUUM FILTER THAT INCREASES THE SOLIDS IN THE UNDERFLOW TO 50 TO 60 PERCENT, SO THAT LESSER AMOUNTS
OF DRY FLY ASH ARE REQUIRED FOR MIXING WITH THE SLUDGE.
                                                  34

-------
OUOUESNE LIGHT
                                                                 ELRAMA  POWER STATION
PERIOD

OCT. 75
  TO
JAN. 76
FEB. 76
MAR.  76
APR.  76
 MAY   76
 JUN.  76
   OPERATING HOURS
BOILER        SCRUBBER VESSELS
            101  201  301  401
            1169
                    1506   976
501
 636
 JUL.  76
 AUG.  76
 SEP. 76
 OCT. 76
 NOV. 76
 DEC. 76
ONE BOILER WAS CONNECTED TO THE SCRUBBER SYSTEM ON
OCTOBER 26, 1975.  A SECOND BOILER WAS CONNECTED
ON FEBRUARY 4, 1976.  FOUR OF THE SCRUBBER VESSELS
HAVE BEEN IN SERVICE IN VARIOUS COMBINATIONS.  THE
SERVICE HOURS TO JANUARY Sli 1974 ARE POSTED IN
THE ACCOMPANYING TABLE.  THE FIFTH VESSEL HAS NOT
BEEN IN SERVICE BECAUSE IT IS BEING REVISED FOR
TRIAL INSTALLATION OF RUBBER-LINED RECYCLE PUMPS.

THE SYSTEM OPERATED DURING THE REPORT PERIOD WITH
a BOILERS COUPLED INTO THE SCRUBBING SYSTEM.  RE-
VISIONS TO THE FIFTH SCRUBBING VESSEL HAVE BEEN
COMPLETED AND OPERATIONS ARE PROCEEDING WITH TWO
RUBBER-LINED RECYCLE PUMPS.

THE SYSTEM IS STILL OPERATING WITH TWO BOILERS
COUPLED INTO THE SCRUBBING SYSTEM.  THE FIFTH
SCRUBBING VESSEL WAS TAKEN OUT OF SERVICE FOR RE-
PAIRS AND MODIFICATIONS REQUIRED FOR THE RUBBER-
LINED RECYCLE PUMPS.  THE UTILITY IS CURRENTLY
CONDUCTING A PERFORMANCE TEST ON THE SCRUBBING
SYSTEM IN THE TWO BOILER OPERATION MODE.  THE IUCS
SLUDGE FIXATION SYSTEM IS STILL OPERATING AT THIS
STATION.

THE FIFTH SCRUBBING VESSEL EMPLOYING TWO RUBBER-
LINED RECYCLE PUMPS WAS OPERATIONAL FOR A SHORT
PERIOD OF TIME DURING THE REPORTING MONTHS.  TWO
BOILERS REMAIN COUPLED INTO THE SCRUBBING SYSTEM.
THE CONSTRUCTION OF ADDITIONAL EQUIPMENT AT THIS
FACILITY IS CONTINUING.  ADDITIONAL LIME STORAGE
SILOS AND A THICKENER WILL BE REQUIRED FOR FULL
SCALE OPERATION.  THE UTILITY HAS SIGNED A LETTER
OF INTENT WITH lues FOR A LONG-TERM SLUDGE FIX-
ATION SYSTEM.  HIGH CALCIUM LIME IS STILL BEING
EMPLOYED IN THE SCRUBBING SYSTEM.

OPERATIONS AT THIS STATION DURING THE REPORT
PERIOD PROCEEDED WITH TWO BOILERS COUPLED INTO
THE 5-MODULE SCRUBBING SYSTEM.  THE 5TH SCRUBBING
VESSEL WAS OPERATIONAL DURING THE REPORT PERIOD
WITH THE RUBBER-LINED RECYCLE PUMPS IN SERVICE.
TESTS WERE CONDUCTED DURING THE PERIOD TO DETER-
MINE PARTICULATE AND S02 REMOVAL EFFICIENCIES.
S02 REMOVAL EFFICIENCY WAS 50 PERCENT.  PARTICU-
LATE EMISSIONS WERE BEING REDUCED WELL BELOW
0.1 LB/MM BTU STANDARD (ACTUAL RESULTS : 0.01
LB/MM BTU).  THESE RESULTS WERE BASED ON 2 BOILERS
COUPLED INTO THE 5 SCRUBBING MODULES WHILE BURNING
MEDIUM-SULFUR (1.0 TO 2.8 PERCENT) COAL.  THE
MECHANICAL COLLECTORS AND ESP'S WERE IN SERVICE
DURING THE TESTS.  OPERATIONS ARE STILL PROCEEDING
ON AN OPEN WATER-LOOP BASIS.  PART OF THE THICKEN-
ER OVERFLOW IS STILL BEING DIVERTED TO THE ASH
POND AND NOT RECYCLED BACK TO THE PROCESS.  BE-
CAUSE BOTH THE BEAVER VALLEY AND BRUCE MANSFIELD
STATIONS ARE FULLY OPERATIONAL, THIS STATION HAS
BEEN RELEGATED TO PEAK LOAD OPERATIONS.  GENERAL
LOAD OPERATIONS ARE FULL LOAD CAPACITY IN THE
DAYTIME AND 50 TO 60 PERCENT LOAD REDUCTION AT
NIGHT.

THE SCRUBBER REMAINED IN SERVICE THROUGHOUT THE
REPORT PERIOD WITH TWO BOILERS COUPLED INTO THE
SCRUBBING SYSTEM.  RECYCLE PUMP EVALUATION IS
BEING CONDUCTED BY THE UTILITY AT BOTH THE PHIL-
LIPS AND ELRAMA STATIONS.  OBSERVATIONS OF THE
RUBBER-LINED RECYCLE PUMPS INDICATE SOME SEVERE
ABRASION AND GOUGING HAVE OCCURRED AFTER 1000
HOURS OF SERVICE TIME.
                                                   35

-------
DUQUESNE LIGHT                                                  ELRAMA POWER STATION

               OPERATING HOURS
PERIOD      BOILER        SCRUBBER VESSELS
                        101  201  301  401  501

     77                                           THE SCRUBBER PLANT CONTINUED OPERATIONS DURING THE
     77                                           REPORT PERIOD WITH TWO BOILERS COUPLED INTO THE
MAR. 77                                           SYSTEM.  TESTING ON THIOSORBIC LIME WAS CONDUCTED
                                                  DURING THE PERIOD.  INSTALLATION OF THE ADDITIONAL
                                                  THICKENER, LIME FEEDERS AND SILOS IS STILL IN
                                                  PROGRESS,  FULL COMPLIANCE OPERATION FOR THIS
                                                  STATION IS SCHEDULED FOR EARLY 1978.  THE FULL
                                                  COMPLIANCE STRATEGY WILL CONSIST OF THE FOLLOWING:
                                                  83X 803 REMOVAL FOR ax SULFUR COAL UTILIZING
                                                  THIOSORBIC LIME C6-13X MG), FIXATING THE SCRUBBER
                                                  SLUDGE WITH THE IUCS POZ-0-TEC STABILIZATION
                                                  METHOD AND HAULING THIS MATERIAL TO AN OFF-SITE
                                                  DISPOSAL/LANDFILL AREA.  CURRENT 303 AND PARTICU-
                                                  LATE REMOVAL EFFICIENCIES ARE 50 AND 99 + X, RE-
                                                  SPECTIVELY.  THE INTERIM IUCS UNIT NOW IN SERVICE
                                                  CONSISTS OF THE OLD MOHAVE PROTOTYPE PLUS A
                                                  VACUUM FILTER.   THE STABILIZED MATERIAL HAS BEEN
                                                  UTILIZED IN A PARKING LOT CONSTRUCTION PROJECT.
                                                  IUCS HAS BEEN AWARDED A 10-YEAR CONTRACT FOR THE
                                                  CONTINUED USE OF THIS SYSTEM FOR FUTURE PLANT
                                                  OPERATIONS.

APR. 77                                           CONSTRUCTION OF TWO 120-FOOT DIAMETER THICKENERS
MAY  77                                           IS CONTINUING.   DUE TO THE GOUGING OF THE RUBBER-
                                                  LINED RECYCLE PUMPS DURING THEIR TESTINGf THEY
                                                  HAVE BEEN REMOVED.  THE UTILITY IS CONSIDERING
                                                  TRYING ANOTHER  SET OF RUBBER-LINED PUMPS.
                                                  DUOUESNE LIGHT  ALSO IS CONTINUING EFFORTS TO
                                                  OBTAIN ALTERNATE LANDFILL AREAS FOR SLUDGE DIS-
                                                  POSAL.

JUN. 77                                           DUQUESNE LIGHT  REPORTED THE FOLLOWING ITEMS FOR
JUL. 77                                           THE ELRAMA SCRUBBER PLANT DURING THE REPORT PERIOD
                                                    *  TWO BOILERS (300 MW) WERE COUPLED INTO THE
                                                       SCRUBBER PLANT.
                                                    *  THE INTERIM IUCS STABILIZATION UNIT (MOHAVE
                                                       PROTOTYPE) CONTINUED TO FIXATE SCRUBBER
                                                       WASTES.
                                                    *  CONSTRUCTION OF THE TWO ADDITIONAL THICKENERS
                                                       CONTINUED  (CONSTRUCTION IS ON SCHEDULE).
                                                    *  FULL PLANT COMPLIANCE IS PROJECTED FOR FEB-
                                                       RUARY 1978.
                                                    *  S02 REMOVAL EFFICIENCY IS APPROXIMATELY 50*.
                                                    *  ELRAMA IS  OPERATING IN A BASE/INTERMEDIATE
                                                       LOAD MODE  (FULL LOAD DAYTIME/HALF LOAD NIGHT-
                                                       TIME).  1976 CAPACITY FACTOR WAS 69.5X.

AUG. 77                                                DURING THE REPORT PERIOD:
SEP. 77                                             *  THE TWO ADDITIONAL THICKENERS WERE COMPLETELY
                                                       INSTALLED.
                                                    *  THE IUCS SYSTEM WAS UPGRADED.
                                                    *  END OF CONSTRUCTION IS PROJECTED FOR FEBRUARY
                                                       1978.
                                                    *  FULL PLANT COMPLIANCE IS PROJECTED FOR APRIL
                                                       1978.

OCT. 77                                                MODULE 101 rtAS UNAVAILABLE OCTOBER 4 DUE  TO
                                                       A BLEED VALVE LEAK AND WAS TAKEN OUT OF SER-
                                                       VICE AT THE END OF THE MONTH FOR CLEANUP.
                                                       MODULE aoi WAS AVAILABLE FOR THE COMPLETE
                                                       MONTH.  MODULE 301 AND 401 HAD OUTAGES IN
                                                       OCTOBER DUE TO RUBBER LINING FAILURE ON I.D.
                                                       FAN.  MODULE 501 HAD RECYCLE PUMP OUTAGES IN
                                                       LATE NOVEMBER.
                                                    *  NEW RUBBER LINED WORMEN RECYCLE PUMPS WERE
                                                       INSTALLED.
                                                    *  LIME HANDLING SYSTEM INSTALLATION CONTINUES.
                                                    *  TUBE LEAKS FORCED BOILER OUTAGE IN NOVEMBER.
                                                    *  LAST TWO BOILERS EXPECTED TO TIE INTO FGD
                                                  36

-------
DUOUESNE LIGHT                                                   ELRAMA  POWER  STATION
                         101  201   301   401   501         SYSTEMS  IN  JANUARY  1978.

               OPERATING HOURS
PERIOD      BOILER         SCRUBBER  VESSELS
                         101  201   301   401   501

NOV. 77                    0   64   672   162   426    MODULE  101, 201  AND 401  HAVE LOW  OPERATIONAL  HOURS
                                                   BECAUSE  ONLY  2 BOILERS  ARE  TIED  INTO  F6D  SYSTEM  TO
                                                   DATE.   THE  SLUDGE  HANDLING  SYSTEM IS  WORKING  WELL.

DEC. 77
JAN. 78
       SCRUBBER  HOURS  WERE NOT  REPORTED BY  THE UTILITY  FOR THIS PERIOD. HOWEVERi  THEY WILL  BE AVAIL-
       ABLE FOR  THE  NEXT UPDATE.
       DURING  THE  PERIOD A NEW  WORMER  RECYCLE PUMP INSTALLED  IN NOVEMBER  EXPERIENCED  JACK SHAFT
       BEARING PROBLEMS  RESULTING  IN THE REMOVAL  OF  SCRUBBER  TRAIN 501  FROM SERVICE.  BOILER NO. 4
       WAS CONNECTED ADDING  AN  ADDITIONAL 176 MW  TO  THE FGD SYSTEM.   THE  IUCS SLUDGE  DISPOSAL
       FACILITY  IS  IN  SERVICE PRODUCING GOOD PRODUCT.   LOW LOAD AND  COAL  STRIKE  HAVE  HAMPERED GOOD
       SCRUBBER  OPERATIONS.  THERE  IS  SOME  OUTAGE TIME  SCHEDULED FOR MARCH.
                                                   37

-------
                  TABLE 3
PERFORMANCE DESCRIPTION FOR OPERATIONAL FGD SYSTEMS THROUGH  01/78
 UTILITY NAME

 UNIT NAME

 UNIT LOCATION

 UNIT RATING

 FUEL CHARACTERISTICS

 FGO VENDOR

 PROCESS

 NEW OR RETROFIT

 START UP DATE

 FGD STATUS

 EFFICIENCY,
  PARTICULATES
 DUOUESNE  LIGHT

 PHILLIPS  POWER  STATION

 SOUTH HEIGHT  PENNSYLVANIA

  410 MW

 COAL   1.0- S.8 PERCENT SULFUR

 CHEMICO

 LIME SCRUBBING

 RETROFIT

  7/73

 OPERATIONAL


 99 PERCENT
  S02


 MATER MAKE UP
                       83 PERCENT DESIGN - 2X S COAL
                       OPEN LOOP
 SLUDGE DISPOSAL
                       HAULAWAY TO OFF SITE LANDFILL
 UNIT  COST
  OPERATIONAL
   EXPERIENCE
SEE APPENDIX A,  FGD SYSTEM ECONOMICS
 REFER TO THE BACKGROUND INFORMATION SECTION IN TABLE 3 OF THIS REPORT.
 THIS SCRUBBING SYSTEM HAS BEEN IN SERVICE SINCE JULY 1973. ALL 6 BOILERS
 ARE COUPLED INTO THE SCRUBBING SYSTEM.   THE PLANT FIRES COAL WITH A HEAT-
 ING VALUE Of HiOOO BTU/LB AND ASH AND  SULFUR CONTENTS OF 31 PERCENT AND
 1.0 - 2.8 PERCENT,  RESPECTIVELY.   DEWATERED SLUDGE FROM THE IUCS INTERIM
 PROCESSING PLANT IS BEING HAULED  TO AN  OFF-SITE LANDFILL.  THE SLUDGE
 CONTAINS NO FIXATIVE.
                                               38

-------
                                       BACKGROUND  INFORMATION
                                                 ON
                                       PHILLIPS POWER  STATION

     THE PHILLIPS POWER STATION IS LOCATED ON  THE  OHIO  RIVER ABOUT  £0  MILES  NORTHWEST  OF  PITTSBURGH.
THE POWER STATION CONSISTS OF SIX COAL-FIRED BOILERS HAVING  A  NET GENERATING CAPABILITY OF  387  MW.
THE RESULTANT FLUE GASES ARE DISCHARGED TO A COMMON HEADER,  TO WHICH  THE  FGD MODULES ARE  CONNECTED
THROUGH ISOLATION VALVES.  THE BOILERS ARE CURRENTLY BUKNING COAL WITH A  HEATING  VALUE OF  11,350 BTU
PER POUND AND SULFUR AND ASH CONTENTS OF Z.Z AND 18.2  PERCENT,  RESPECTIVELY.

     THE FGD SYSTEM, WHICH SUPPLEMENTS THE EXISTING MECHANICAL AND  ELECTROSTATIC  OUST  COLLECTORS,
CONSISTS OF FOUR TRAINS OF WET VENTUR1-TYPE SCRUBBERS,  INSTALLED AT A  COST OF APPROXIMATELY  S103/KW.
GIBBS & HILL., WAS ENGAGED AS THE A-E FIRM FOR THE ENTIRE  PROJECT.  BATTERY  LIMITS  OF  THE  CHEMICO
CORPORATION ARE CONFINED TO THE SCRUBBERS AND  ASSOCIATED PUMPS AND  CONTROLS  BETWEEN THE INLET HOT
GAS DUCT MANIFOLD AND THE EXIT WET GAS HEADER  (INCLUDING THE REHEATER,  EXCLUDING  THE NEW  ID  FANS).

     THE FOUR TRAINS ARE LOCATED DOWNSTREAM OF EXISTING MECHANICAL  COLLECTORS AND ESP'S INSTALLED IN
SERIES ON EACH OF THE SIX PULVERIZED-COAL-FIRED BOILERS.   THREE OF  THE TRAINS ARE SINGLE-STAGE
VENTURI SCRUBBERS ORIGINALLY INTENDED FOR PARTICULATE  REMOVAL.  THE FOURTH TRAIN  IS A  DUAL-STAGE
VENTURI SCRUBBER-ABSORBER AND IS THE PROTOTYPE FOR DETERMINING THE  FEASIBILITY  OF TWO-STAGE  SCRUB-
BING FOR COMPLIANCE WITH SULFUR DIOXIDE EMISSION LIMITS. A DIAGRAM  OF  THE SCRUBBER-ABSORBER  TRAIN
INSTALLED AT THE PHILLIPS STATION IS PRESENTED IN  APPENDIX B.

     EACH TRAIN IS EQUIPPED WITH A NEW WEI-TYPE ID FAN.  A NEW COMMON  DUCT DIRECTS  GAS STREAMS  FROM
AIR BOILERS TO THE SCRUBBER SYSTEM, WHERE THEY CAN BE  SENT TO  ANY OR  ALL  OF  THE TRAINS.   THE SCRUB-
BED GAS IS EXHAUSTED THROUGH A COMMON DUCT AND AN  OIL-FIRED  REHEATER  TO A NEW GROUND-SUPPORTED
STACK WHICH CONTAINS AN ACID-RESISTANT BRICK LINER.

     SLAKED QUICKLIME IS ADDED TO THE LOWER CONE OF EACH OF  THE SCRUBBER  VESSELS  TO NEUTRALIZE  THE
RECIRCULATING LIQUOR, WHICH, IN SINGLE-STAGE SCRUBBING  WITH  HIGH-CALCIUM  LIME,  REACTS  WITH  APPROX-
IMATELY 50 PERCENT OF THE SULFUR DIOXIDE IN THE FLUE GAS.  A LIQUOR BLEED FLOW  OF APPROXIMATELY 4
PERCENT IS SENT TO ONE OR BOTH OF THE THICKENERS FOR REMOVAL OF SOLIDS.  THE OVERFLOW  IS  RETURNED TO
THE SYSTEM AND THE UNDERFLOW IS DISCHARGED TO  THE  IUCS  SLUDGE  FIXATION SYSTEM.  THIS INTERIM SLUDGE
FIXATION SYSTEM COMMENCED OPERATIONS IN DECEMBER 1976.  THE  FACILITY  INCLUDES DEWATERING .EQUIPMENT
AND FLY ASH ADDITION EQUIPMENT (COLLECTED FROM THE ESP).   THE  FIXATED  MATERIAL  IS THEN HAULED AWAY
TO AN OFF-SITE LANDFILL AREA.

     FLUE GASES FROM THE BOILERS ARE ACCELERATED TO A  HIGH VELOCITY IN THE SCRUBBER.   AT  THE THROAT,
THE GASES COLLIDE WITH THE SCRUBBING LIQUID, ATOMIZING  IT  INTO SMALL  DROPLETS.  THE FLY ASH  AND THE
SULFUR  DIOXIDE IN THE GAS ARE REMOVED BY THE SLURRY DROPLETS AND EXIT  AT  THE BASE OF THE  TOWER.  THE
GAS THEN REVERSES DIRECTION AND FLOWS UP THROUGH THE MIST  ELIMINATOR,  WHERE  FINE  DROPLETS  ARE REMOV-
ED BEFORE THE GAS LEAVES THE SCRUBBER.

     STARTUP  OF A PORTION OF THE PHILLIPS SCRUBBER SYSTEM  BEGAN JULY  1973.   SEVERAL PROBLEMS THEN
DEVELOPED IN  THE FORM OF EROSION OF FANS AND THE LIME  FEED SYSTEM,  CAUSING OUTAGES  OF  THE  SCRUBBER
SYSTEM.  AFTER AN EXTENDED OUTAGE, THE SCRUBBER SYSTEM  WAS RETURNED TO SERVICE  IN MARCH 1974.   THE
SYSTEM  HAS BEEN OPERATING CONTINUOUSLY SINCE THAT  TIME  WITH  VARIOUS NUMBERS  OF  BOILERS CONNECTED TO
THE SCRUBBER  SYSTEM  AND SCRUBBER TRAINS IN SERVICE.

     DETERMINATION OF THE AVAILABILITY OF THE  PHILLIPS  SYSTEM  HAS BEEN DIFFICULT.   UNTIL  ALL BOILERS
WERE CONNECTED TO THE SCRUBBERS, THERE WAS AT  LEAST ONE SPARE  TRAIN AND AS MUCH AS  100 PERCENT  SPARE
SCRUBBER CAPACITY.   THEREFORE, HAVING A TRAIN  OUT  OF SERVICE FOR MAINTENANCE DID  NOT REDUCE  THE CAP-
ABILITY  OF THE SCRUBBER SYSTEM.  UNTIL ALL SIX BOILERS  WERE  CONNECTED,  MEANINGFUL AVAILABILITY
FACTORS COULD NOT BE COMPUTED.  ON MARCH 17, 1975, THE  SIXTH BOILER WAS CONNECTED,  AND ALL  FOUR
SCRUBBER TRAINS WERE REQUIRED TO BE IN SERVICE.  OPERATION IN  THAT  MODE CONTINUED UNTIL AUGUST  4,
1975,  WHEN THE NO. 6 BOILER WAS REMOVED FROM THE SCRUBBER  SYSTEM BECAUSE  THE PH LEVEL  COULD  NOT 8E
MAINTAINED AND DEPOSITS BECAME UNMANAGEABLE TO THE POINT THAT  SCRUBBER OUTAGES  WERE REDUCING GENERA-
TING CAPABILITY OF THE STATION. ADDITIONAL INFORMATION  AND DATA ON  SUBSEQUENT BOILER AND  SCRUBBER
PLANT  OPERATIONS ARE PROVIDED IN A CHRONOLOGICAL FASHION IN  THE TABLE  THAT FOLLOWS.
                                                   39

-------
DUQUESNE LIGHT                                                        PHILLIPS  POWER  STATION

                          OPERATING HOURS
                    BOILER                          SCRUBBER-ABSORBER
MONTH      2     2     3     a      5      6      101    201    301    401

JUL. 75   83   644   703   319    605    643      400    180    531    723
       FOURTH FGD TRAIN AND SIXTH BOILER WERE TIED IN ON MARCH 17,  1975.  PARTICIPATE  TESTS IN MAY
       SHOWED OUTLET LOADINGS OF 0.04 LB/MILLION BTU.  THE TWO-STAGE  TRAIN HAS BEEN  OUT  OF  SERVICE
       FROM JUNE 19 FOR GENERAL CLEANING AND REPAIR OF A LEAK IN THE  FIRST-STAGE  SCRUBBER.

AUG. 75  354   701   454   457    517    445      478    682    323    319
       SCRUBBER UNAVAILABILITY FORCED RETURNING BOILER NO. 6 TO THE SCRUBBER BYPASS  GAS  PATH  TO
       PREVENT LOSS OF BOILER CAPACITY.  PLUGGING AND MAINTENANCE PROBLEMS HAVE BEEN ENCOUNTERED.
       EVALUATION OF VARIOUS RECYCLE PUMPS IS CONTINUING.

SEP. 75  463   287   669   503    672    525       57    561    685    536

OCT. 75  547   575   620   604    681    687      607    207    505    487
       IN OCTOBER 1975, PHILLIPS INITIATED THIOSORBIC LIME SCRUBBING  IN THEIR  SINGLE-STAGE  MODULES
       ON AN EXPERIMENTAL BASIS.  THE PURPOSE IS TO STUDY COMPLIANCE  FEASIBILITY,  S02 REMOVAL
       EFFICIENCY, AND OUALITY OF THE SLUDGE GENERATED BY THE SINGLE-STAGE MODULES.

NOV. 75   16   720   688    70    720    593      626    720      0     75

DEC. 75  172   660   709     0    689    547      360    661    182    386
       THE UTILITY CONCLUDED THE THIOSORBIC LIME TESTING PROGRAM IN MID-DECEMBER.  FOUR  BOILERS WERE
       COUPLED TO THE SCRUBBING SYSTEM DURING THE RUN.  THE UTILITY IS NOW ANALYZING THE  DATA
       GENERATED DURING THE TEST PROGRAM.  THE SCRUBBERS HAVE BEEN PUT BACK ON REGULAR LIME.   NO
       UNUSUAL PROBLEMS WERE ENCOUNTERED DURING THE TEST RUN.

JAN. 76  222   722   639     0    662    661      277    536    101    707
       THE 2.5-MONTH TEST PROGRAM WITH THIOSORBIC LIME INCLUDED 1612  HOURS ON  ONE TRAIN  AND 1309
       HOURS ON ANOTHER TRAIN.  RESULTS  INDICATE THAT THE REQUIRED DEGREE OF S02  REMOVALC83 PERCENT)
       CAN BE OBTAINED WITH AN MGO CONTENT OF 6-10 PERCENT IN THE LIME WITH SINGLE-STAGE  SCRUBBING.

FEB. 76  445   588   672     0    633    571      657    662    166    406

MAR. 76                                           695    353    659    461

APR. 76
       PLANT OPERATION IS PROCEEDING WITH A TOTAL OF 4 BOILERS COUPLED INTO THE SCRUBBING SYSTEM
        (EQUALING 336 MW, WHICH IS 87 PERCENT OF THE TOTAL PLANT CAPACITY).  THE FGD  SYSTEM  OPERATED
       ON HIGH CALCIUM LIME DURING THE REPORT PERIOD.  THE GENERAL OPERATION MODE AT THIS FACILITY
       HAS ONE OF THE FOUR SCRUBBING TRAINS OUT CONTINUALLY FOR REPAIRS, CLEANING, AND PREVENTIVE
       MAINTENANCE.  THE UTILITY IS STILL EXPERIENCING PROBLEMS WITH  SOLIDS DEPOSITION IN THE
       VENTURI THROAT OF THE SCRUBBING MODULE, CAUSING MOVEMENT INHIBITION AND GREATER PRESSURE
       DROPS.  THE FGD SYSTEM AVAILABILITY FOR THE FIRST QUARTER OF 1976 WAS 72 PERCENT.  THE  SLUDGE
       STABILIZATION PRACTICES ARE STILL CONTINUING AT THIS FACILITY.

MAY  76

JUN. 76
       REDUCED LOAD OPERATIONS WERE REPORTED BY THE UTILITY FOR THE MAY-JUNE PERIOD  BECAUSE OF A
       SCHEDULED TURBINE OVERHAUL TO UNIT NO.6.  THE SCRUBBING SYSTEM WAS SHUT DOWN  ON JUNE 27 FOR A
       SCHEDULED FOUR WEEK REPAIR PERIOD.  THE MAJORITY OF THE WORK WILL BE CONCENTRATED  ON THE
       STACK, ASSOCIATED DUCTWORK AND BOILER DAMPERS.  ALSO, THE UTILITY IS PROCEEDING WITH THE
        INSTALLATION OF 3 ADDITIONAL LIME STORAGE SILOS AND A THIRD THICKENER.

JUL. 76

AUG. 76
       THE 4-WEEK SYSTEM OVERHAUL WAS COMPLETED JULY 25.  DURING THIS PERIOD,  THE FOLLOWING REPAIRS
       AND MODIFICATIONS WERE MADE!
               •REPAIR OF THE TURNING VANES TO THE SCRUBBER DEMISTER.
               •REPAIR OF THE EXPANSION  JOINT SEAL WHERE THE DUCTWORK TIES INTO THE  MAIN  STACK.
               •REPAIR OF STEEL BANDS AROUND INNER STACK STRUCTURE.
               •OVERHAUL OF I.D. FANS.
               •REPAIR OF BOILER EXIT DAMPERS.
               •REPAIR LEAKAGE OF THE ACID-BRICK LINING IN THE MAIN STACK.
       THE THREE ADDITIONAL LIME STORAGE SILOS AND THE FOUNDATION FOR THE ADDITIONAL 75-FOOT
       DIAMETER THICKENER HAVE BEEN INSTALLED.  THE UTILITY HAS SIGNED A LETTER-OF-INTENT WITH IUC3.
       FOR A LONG-TERM SLUDGE TREATMENT  SYSTEM.
                                                  40

-------
OUQUENSE LIGHT
                                                                 PHILLIPS POWER STATION
                          OPERATING  HOURS
MONTH

SEP. 76
   BOILER
a     3
  SCRUBBER-ABSORBER
101     201    301    401
OCT. 76
       BOILER NOS. 2-6  WERE  COUPLED  INTO  THE  SCRUBBING SYSTEM.   BOILER NO. 1 IS DOWN FOR OVERHAUL
       AND REPAIRS.   THE  IUCS  INTERIM  SLUDGE  PROCESSING PLANT IS UNDER CONSTRUCTION AND WILL BE IN
       SERVICE BY DECEMBER  1976.   THE  TEMPORARY FACILITIES WILL PROCESS THE THICKENER UNDER FLOW AND
       PONDED  SLUDGE UNTIL  THE  POND IS DEPLETED OF SLUDGE AND  THE PERMANENT FACILITY HAS BEEN
       INSTALLED.  SCRUBBING OPERATIONS ARE STILL PROCEEDING IN AN OPEN-WATER-LOOP MODE WITH PART OF
       THE THICKER OVERFLOW  BEING  DIVERTED TO THE ASH POND.  BECAUSE BOTH THE BEAVER VALLEY AND
       BRUCE MANSFIELD  STATIONS  ARE  FULLY OPERATIONAL, THIS STATION HAS BEEN RELEGATED TO PEAK LOAD
       OPERATIONS.   GENERAL  LOAD OPERATIONS ARE FULL LOAD CAPACITY IN THE DAYTIME AND 50 TO 67
       PERCENT LOAD  REDUCTION  AT NIGHT.
            TOTAL  SCRUBBER  HOURS;  23,274
            TOTAL  BOILER  HOURS;  83,642
            TOTAL  SCRUBBER  OUTAGE  TIME;  5,500
            TOTAL  SCRUBBER  AVAILABILITY  HOURS;
            23,274
            AVERAGE  MW  LOAD/  SCRUBBER OPERATION
             HOUR; 243
             TOTAL OPERABILITY  INDEX; 28 PERCENT
             TOTAL RELIABILITY  INDEX; ei PERCENT
                                 THE FIGURES  IN  THE LEFT-HAND  COLUMNS HAVE BEEN
                                 COMPILED BY  THE  UTILITY  FOR SYSTEM  OPERATIONS FOR
                                 THE PERIOD FOLLOWING  START-UP  IN  JULY  1973
                                 INCLUSIVE TO OCTOBER  1976.  THE TOTAL  SCRUBBER
                                 HOURS  VALUE  INCLUDE OPERATION  TIME  WHEN ONE OR
                                 MORE OF THE  MODULES WERE  IN SERVICE.   TOTAL BOILER
                                 AND UNAVAILABILITY VALUES APPLY FOR ALL THE COR-
                                 RESPONDING UNITS.  THE TOTAL  SCRUBBER  AVAILABILITY
                                 INDEX  INCLUDES  THE TIME  WHEN  ONE  OR MORE MODULES
                                 WERE AVAILABLE  FOR SERVICE.
 NOV.  76

 DEC.  76
        THE UTILITY REPORTS THAT BOILERS 2-b REMAINED COUPLED INTO THE SCRUBBING SYSTEM DURING THE
        REPORT PERIOD.   THE INTERIM IUCS FIXATION FACILITY WAS INSTALLED AND COMMENCED OPERATIONS
        IN DECEMBER.  THE UTILITY REPORTS THAT THE VENTURI SCRUBBERS AHE STILL DEVELOPING LARGE
        AMOUNTS OF SCALE ON THE INTERNALS,  RESULTING IN TWICE NORMAL PRESSURE DROPS.   THE RECYCLE
        PUMP EVALUATION HAS BEEN IN PROGRESS.  APPROXIMATELY 2500 TO 2800 HOURS OF OPERATION TIME
        HAVE BEEN ACCUMULATED ON THE VARIOUS UNITS WITH NO FAILURES OH APPRECIABLE WEAR OBSERVED.
        THE ADDITIONAL  OEWATERING AND REAGENT PREPARATION EQUIPMENT IS NOW BEING INSTALLED. THE
        CONTRACT HAS BEEN AWARDED TO DRAVO  TO PROVIDE THIOSORBIC LIME FOR THIS SCRUBBING SYSTEM.  ALL
        BOILERS HAVE BEEN HEADERED INTO THE SCRUBBER PLANT.  A NUMBER OF THE UNITS WERE DOWN FOR
        OVERHAUL AND REPAIR THE INTERIM IUCS POZ-0-TEC UNIT REMAINED IN SERVICE, FILTERING OUT WATER
        ONLY.  THE RECYCLE PUMP EVALUATION  IS CONTINUING.  AFTER 4000 HRS. OF OPERATION.  THE CARBOR-
        UNDUM IMPELLERS AND WEAR RINGS STILL LOOK GOOD.  S02 AND PARTICULATE REMOVAL  EFFICIENCIES
        ARE 50 & 99 + X  RESPECTIVELY.  INSTALLATION OF THE ADDITIONAL SILOS, THICKENERS, AND LIME
        FEEDERS IS STILL IN PROGRESS.  FULL COMPLIANCE PLANT OPERATIONS ARE SCHEDULED FOR DEC.
 JAN. 77

 FEB. 77

 MAR. 77
        1977 FULL COMPLIANCE OPERATIONS WILL INCLUDE 83X S02 REMOVAL FOR 2X SULFUR COAL UTILIZING
        THIOSORBIC LIME (6-12XMG) & FIXATING THE SCRUBBER WASTES WITH THE IUCS POZ-0-TEC METHOD.
        THE FIXATED MATTER WILL BE HAULED AWAY TO AN OFF-SITE DISPOSAL AND LANDFILL.  IUCS HAS BEEN
        AWARDED A 10 YEAR CONTRACT FOR THE USE OF THIS METHOD.  THE CARBORUNDUM IMPELLORS AND WEAR
        RINGS CONTINUE TO LOOK GOOD AFTER MORE THAN 5000 HOURS OF OPERATION.
 APR. 77
 MAY. 77
        THIOSORBIC LIME TESTS BEGAN IN LATE MAY BUT LASTED ONLY ABOUT ONE WEEK.  THE  SCRUBBER SYSTEM
        WAS SHUT DOWN FOR 3 TO 4 DAYS IN MAY DUE TO LEAKING IN THE WET DUCT HEADER THAT LEADS TO THE
        STACK.  WHILE FIXING THE LEAK, INSPECTION OF OTHER COMPONENTS REVEALED THAT THE BOILER EXIT
        DAMPERS WERE ERODING.  ONE 201 EXTERNAL MIST ELIMINATOR ALSO WAS SEVERLY ERODED AND PLUGGED
        ONCE THE LEAK TO THE HEADER WAS REPAIRED, FLUE GAS FROM FOUR BOILERS BEGAN TO BE SCRUBBED.
        TWO OF THE SIX BOILERS ARE DOWN FOR MAINTENANCE.  THE DAMPERS AND MIST ELIMINATOR REPAIRS
        WILL BE CORRECTED AT A SCHEDULED OUTAGE TIME.  OVERALL SCRUBBER AVAILABILITY IS ABOUT 75 PER-
        CENT. THE INTERIM SLUDGE DISPOSAL SYSTEM STILL IS OPERATIONAL.  THE PERMANENT SLUDGE DISPOSAL
        FACILITY IS ON SCHEDULE FOR THE DECEMBER 1977 COMPLETION DATE.
 JUN. 77

 JUL. 77
        ALL 6 BOILERS ARE COUPLED INTO THE SCRUBBER PLANT.  FLUE GAS FROM 5 OF THESE UNITS IS BEING
        TREATED BY THE SCRUBBERS.  UNIT NO. 6 HAS BEEN DOWN FOR AN EXTENDED TURBINE REPAIR OUTAGE.

-------
DUQUENSE LIGHT
                                                                PHILLIPS  POWER  STATION
MONTH
           1
              BOILER
                 3
                          OPERATING HOURS
                                               SCRUBBER-ABSORBER
                                             101    201    301    401
DEC.
JAN.
       OPERATIONS ARE PROCEEDING WITH ONE SCRUBBING TRAIN BEING SPARED AT ALL  TIMES  (MAINTENANCE
       AND CLEANOUT).  S02 REMOVAL EFFICIENCY IS APPROXIMATELY SOX.  THE RECYCLE  PUMP  EVALUATION
       STUDY CONTINUED DURING THE PERIOD. COMPONENTS BEING EVALUATED INCLUDE*  CARBORUNDUM  IMPELLERS,
       CARBORUNDUM WEAR RINGS, TITANIUM IMPELLERS, 31733 WEAR RINGS STELLITE TIPPED.   A  THIOSORBIC
       LIME TEST WAS PREMATURELY TERMINATED BECAUSE OF SOME MINOR SLAKER/FEEDER PROBLEMS.  HIGH
       CALCIUM VIRGIN LIME WAS UTILIZED DURING THE MAJORITY OF OPERATIONS THROUGHOUT THE PERIOD.
       ONLY 4 OF THE 6 BOILERS ARE OPERATING AS THE TURBINE REPAIR OUTAGE CONTINUES.
AUG. 77

SEP. 77
OCT. 77
NOV. 77
 LIME  HANDLING  AND  SOLID  WASTE  DISPOSAL  FACILITIES  WERE  BEING  SCALED  UP  TO HANDLE FULL
 CAPACITY  AND A  THIRD  THICKENER WAS  INSTALLED  AND BROUGHT  INTO SERVICE DURING THIS REPORT
 PERIOD.   THE IUCS  SYSTEM IS  IN THE  INTERIM  PHASE.   WASTE  WATER IS  BEING MIXED WITH FLYASH AND
 DISPOSED  OF.   CURRENT CONSTRUCTION  WORK IS  EXPECTED TO  BE  COMPLETED  6Y  THE END OF JANUARY
 WHEN  ALL  b  BOILERS WILL  BE  BACK  ON  LINE FOR A TWO  MONTH TEST  PERIOD.  THIOSORBIC LIME IS
 STILL BEING TESTED.   RESULTS  ARE NOT  YET AVAILABLE.   THE  FGD  SYSTEM  WILL BE DOWN FOR THE
 FIRST WEEKEND  OF NOVEMBER.   THE  SYSTEM  WILL ALSO BE  CHECKED FOR  MAIN DUCT LEAKS AT THIS TIME.
 ALSO  THE  SCRUBBER  AND STACK  LININGS AND RECYCLE PUMPS WILL BE THOROUGHLY CHECKED.  NECESSARY
 REPLACEMENTS AND REPAIRS WILL  BE CARRIED OUT. CURRENT  S02 REMOVAL  EFFICIENCY IS 50 PERCENT.
 BY  EARLY  APRIL  THE SYSTEM IS  EXPECTED TO REACH COMPLIANCE  WITH AN  S02 EFFICIENCY OF 83
 PERCENT.

r
 MODULE 101  WAS  DOWN  A TOTAL  OF 113  HOURS IN OCTOBER.  MODULE  201 WAS PUT IN SERVICE ON
 OCTOBER 26  AFTER EXTENSIVE  CLEAN UP AND REPAIRS TO  RUBBER  LINING AND I.D. FAN.  MODULE 301
 WAS DOWN  A  TOTAL OF  57 HOURS  IN  OCTOBER. MODULE aoi  WAS  DOWN A  TOTAL OF 36 HOURS IN OCTOBER
 FOR REPAIRING  HOLES  IN FAN  LINING AND TYING IN THICKENER  BLEED LINE.

1
 DURING SHUTDOWN OUTLET DUCT  LEAKS WERE  REPAIRED.   BOILER  EXIT DAMPERS WERE REPLACED DUE TO
 EROSION BY  FLYASH.  CORROSION  OF STEEL  BANDS  IN STACK WAS  ALSO NOTICED.  DEWATERING OPERATIONS
 ARE NOT WORKING PROPERLY,  CAUSING PROBLEMS  IN SLUDGE  HANDLING.   THE  RESULTS FROM THIOSORBIC
 LIME  USE  CAN NOT YET  BE  QUANTIFIED  DUE  TO LIME FEED  SYSTEM PROBLEMS.
                                                22391  20996
                                       AN OVERHAUL FROM NOV.
                                                       22229   22259
                                                       17 TO MONDAY 2-6-78  WHEN  IT  RETURNED  TO
77
77 (CUMULATIVE HRS.  THRU 1-8-78)
  SCRUBBER TRAIN 301  WAS DOWN FOR
  SERVICE.
  SCRUBBER TRAIN 401  WAS REMOVED  FROM SERVICE  ON  THE  6TH  OF  FEBRUARY.
  THE IUCS INTERIM SLUDGE TREATMENT  SYSTEM  HAS HAD  SOME DEWATERING  PROBLEMS.   DURING DECEMBER
  PHILLIPS EXPERIENCED POOR SLUDGE REMOVAL.   THE  IUCS PLANT  IS  WORKING  ON A  PART  TIME BASIS.
  FULL OPERATIONS ARE EXPECTED LATE  THIS SPRING.
  THE POOR QUALITY SLUDGE IS SENT  TO AN EMERGENCY POND AND  THEN RECIRCULATED  BACK TO THE THICK-
  ENER BUT THIS CAUSES A WATER UNBALANCE IN  THE SYSTEM.
  TESTING WITH THIOSORBIC LIME i>  5»  MGO HAS  SHOWN THAT THE  MGO  CONCENTRATION  IS NOT GREAT
  ENOUGH TO EFFECT ADEQUATE 802 REMOVAL ON  A SINGLE STAGE SCRUBBER.   THEY ARE GOING TO TEST AT
  A GREATER MGO CONCENTRATION BY  STARTING AT 10X  AND  THEN DROPPING  BACK UNTIL THE CONCENTRATION
  IS SATISFACTORY.  THIS TESTING,  AS WELL AS SCRUBBER OPERATIONS, HAVE, HOWEVER,  BEEN HAMPERED
  BY LOW LOADS AS A  RESULT OF THE  COAL STRIKE.
  THERE WILL BE AN OUTAGE AT PHILLIPS TO REPLACE  THE  CARBON  STEEL BANDS WITH  STAINLESS STEEL
  BANDS.
                                                  42

-------
                  TABLE 3
PERFORMANCE DESCRIPTION FOR OPERATIONAL FGD  SYSTEMS  THROUGH   01/78
 UTILITY NAME


 UNIT NAME


 UNIT LOCATION


 UNIT RATING


 FUEL CHARACTERISTICS


 FGO VENDOR


 PROCESS


 NEW OR RETROFIT


 START UP DATE


 FGD STATUS


 EFFICIENCY,
   PARTICULATES
 INDIANAPOLIS  POWER  &  LIGHT CO.


 PETERSBURG NO 3


 PETERSBURG INDIANA


  530  MW


 COAL   3.0-3.5 PERCENT SULFUR


 UNIVERSAL OIL PRODUCTS


 LIMESTONE SCRUBBING


 NEW


 10/77


 OPERATIONAL



 99.3  PERCENT
   S02
                        60  PERCENT  (DESIGN)
  WATER  MAKE  UP
  SLUDGE DISPOSAL
 IUCS SLUDGE STABILIZATION
  UNIT  COST
SEE APPENDIX A,  FGD SYSTEM ECONOMICS
  OPERATIONAL
   EXPERIENCE
 INDIANAPOLIS P & L HAS AWARDED A CONTRACT  TO UNIVERSAL OIL  PRODUCTS  FOR  A
 WET LIMESTONE SCRUBBING S02 CONTROL SYSTEM.   AN ESP PROVIDES PRIMARY PAK-
 TICULATE CONTROL.  THE UNIT FIRES BITUMINOUS COAL  WITH A  SULFUR  CONTENT
 OF 3.0-3.5X, AN ASH CONTENT OF 9-10X,  AND  A  HEAT CONTENT  OF UrOOO
 BTU/LB.  THE FOUR MODULES OPERATED FOR 2«  HOURS IN MID-DECEMBER  FOR
 EQUIPMENT TESTING.  THE SCRUBBERS WERE TAKEN OUT OF SERVICE SO  THAT  SOME
 FINAL ADJUSTMENTS COULD BE MADE.  SCRUBBERS  ARE EXPECTED  TO BE  BACK  IN
 SERVICE BY EARLY MARCH 1978.
                                                43

-------
                                     BACKROUND INFORMATION ON
                                          PETERSBURG NO. 3

     THE PETERSBURG POWER STATION, OWNED AND OPERATED BY THE INDIANAPOLIS POWER AND LIGHT  COMPANY
(IPALCO), IS LOCATED NEAR PETERSBURG, INDIANA, APPROXIMATELY 100 MILES SOUTHWEST OF INDIANAPOLIS.
THE STATION CONSISTS OF THREE COAL-FIRED, STEAM-TURBINE, GENERATING UNITS, WHICH HAVE A COMBINtU
POWER GENERATING CAPACITY OF 1180 MN.  UNIT 1 IS RATED AT 320 MW, UNIT 2 AT 430 MW, AND UNIT  1  Al
530 MW.  THE UTILITY IS PLANNING THE INSTALLATION OF ANOTHER 530-MW UNIT, WHICH IS SCHEDULED  TO Bt
IN SERVICE BY APRIL 1982.  UNIT 4 WILL BRING THE STATION'S COMBINED POWER GENERATING CAPACITY TO
1710 MW.  OF THE THREE OPERATIONAL UNITS, ONLY UNIT 3 IS REQUIRED TO MEET CURRENT FEDERAL  NErtiUUKCE
PERFORMANCE STANDARDS FOR SULFUR DIOXIDE (S02) EMISSIONS (1.2 LB/MM BTU) .  THIS UNIT IS FITTED  WITH
A FLUE GAS DESULFURIZATION (FGD) SYSTEM.

     THE BOILER ON UNIT 3 IS A COMBUSTION ENGINEERING UNIT DESIGNED TO FIRE HIGH-SULFUR INDIANA
BITUMINOUS COAL WITH THE FOLLOWING CHARACTERISTICS: HEAT CONTENT, 10,750 BTU/LB; SULFUR CONTENT,
U.50 PERCENT? ASH CONTENT, 8 TO 15 PERCENT; MOISTURE CONTENT, 10.5 TO 16.5 PERCENT.  THE EMISSION
CONTROL  SYSTEM ON THIS UNIT CONSISTS OF TWO ELECTROSTATIC PRECIPITATORS  (ESP'S) FOR THE CONTROL OF
PARTICULATE MATTER AND AN FGD SYSTEM WITH FOUR WET LIMESTONE SCRUBBER MODULES FOR CONTROL  OF  S02.

     BOILER FLUE GAS, WHICH IS GENERATED AT A RATE OF 1.9 MILLION ACFM AT 279 F, CONTAINS  3.55
GRAINS OF PARTICULATES PER ACTUAL CUBIC FOOT AND 2567 PPM OF S02.  THE GAS FIRST ENTERS ONE OF  THE
TWO RESEARCH COTTRELL COLO-SIDE ESP'S FOR PRIMARY PARTICULATE CONTROL.   THE ESP'S REMOVE 99.3 PER-
CENT OF  THE INLET PARTICULATE MATTER, WHICH RESULTS IN AN OUTLET LOADING OF 0.025 GR/ACF (0.1 LB/MM
BTU).  FOUR FORCED-DRAFT BOOSTER FANS (ONE PER MODULE), EACH WITH AN 18  IN. W.G., THEN BOOST  THE GAS
THROUGH  THE FGD SYSTEM.  THE FOUR TURBULENT CONTACT ABSORBERS (TCA'S) THAT COMPRISE THE FSO SYSTEM
WERE SUPPLIED BY UNIVERSAL OIL PRODUCTS  (UOP) .  THE TOTAL CAPACITY OF THE SYSTEM IS DIVIDED EVENLY
AMONG  THE MODULES, EACH OF WHICH IS  30 FT. BY 30 FT. BY 100 FT. HIGH AND CAPABLE OF TREATING
475,000  ACFM OF FLUE GAS.  LIMESTONE SLURRY IS CONTACTED WITH THE GAS STREAM IN EACH OF THREE LEVELS
OF MOBILE BED PACKING (1,5-INCH-DIAMETER SPHERES) IN EACH MODULE.  MODULE PRESSURE DROP IS 8.5  IN.
W.G.,  SUPERFICIAL GAS VELOCITY IS 14.5 FT/S, AND LIGIUID-TO-GAS (L/G) RATIO IS 60.  TWO 9300-GPM
PUMPS  PROVIDE LIMESTONE SLURRY FOR EACH MODULE (ONE SPARE PUMP PER TWO MODULES).  THE SCRUBBED  FLUE
GAS  (375,000 ACFM AT 118 F), WHICH CONTAINS 385 PPM 802, THEN PASSES THROUGH THE MIST ELIMINATORS
AND  IS REHEATED FROM 118 TO 148 F BEFORE IT IS DISCHARGED THROUGH THE 616-FT MAIN STACK.   REHEAT IS
PROVIDED BY HEATING AMBIENT AIR WITH STEAM TUBE BUNDLES LOCATED OUTSIDE  THE GAS DUCTS.

     THE SPENT SCRUBBING SOLUTION IS DISCHARGED FROM THE TCA MODULES TO  AN EXTERNAL RECYCLE TANK,
WHERE  CHEMICAL REACTIONS ARE COMPLETED.  FLUE GAS CLEANING WASTES (CALCIUM SULFITE, CALCIUM SULFATE,
CALCIUM  CARBONATE, FLY ASH) ARE DISCHARGED FROM THE LIQUID RECIRCULATION LOOP TO A THICKENER  (165 FT
IN DIAMETER), WHERE THE WASTE SOLIDS SETTLE OUT.  THICKENER OVERFLOW IS  SENT TO A THICKENER OVERFLOW
RECLAIM  WATER TANK FOR RETURN TO THE PROCESS; 150 TONS/HOUR OF THICKENER UNDERFLOW, WHICH  IS  35
PERCENT  SOLIDS, IS DISCHARGED TO AN  IUCS SLUDGE STABILIZATION SYSTEM FOR CHEMICAL FIXATION BEFORE
BEING  PIPED TO FINAL DISPOSAL IN AN  ON-SITE, UNLINED, DISPOSAL POND LOCATED APPROXIMATELY  4000  FT
FROM THE GENERATING UNIT.  CLARIFIED WATER IS RETURNED TO THE PROCESS FOR FURTHER USE.

     A BALL MILL WITH A CAPACITY OF  50 TONS/HR PROVIDES ON SITE LIMESTONE PREPARATION.  THE MILL IS
FED  DIRECTLY FROM A 400-TON LIMESTONE STORAGE SILO.  THE CRUSHED LIMESTONE IS SLURRIED TO  A 38  PER-
CENT SOLIDS SOLUTION AND STORED IN 320,000-GAL MIX/HOLD TANKS.  TWO PUMPS TRANSFER FRESH SLURRY FROM
THE  STORAGE TANKS TO THE RECIRCULATION TANKS.  THE MODULES, TANKS, AND PUMPS IN THE FGD SYSTEM  ARE
RUBBER-LINED.  EXHAUST GAS DUCTWORK  IS LINED WITH A CEILCOTE LINER.

"INITIAL OPERATING EXPERIENCE*

     BY  DECEMBER 12, 1977, IPALCO HAD PUT THE FIRST TWO TCA MODULES INTO OPERATION.  THE OTHER  TWO
MODULES  WERE PLACED ON LINE THE LATTER PART OF THE SAME MONTH.  SEVERE COLD WEATHER CONDITIONS  HAVE
NECESSITATED THE ERECTION OF TEMPORARY ENCLOSURES AROUND SEGMENTS OF THE FGD SYSTEM UNTIL  THE
INSTALLATION OF HEAT TRACING IN THE  LIQUID CIRCUIT IS COMPLETED.
                                                  44

-------
                  TABLE 3
PERFORMANCE DESCRIPTION FOR OPERATIONAL FGD  SYSTEMS  THROUGH   01/78
 UTILITY NAME

 UNIT NAME

 UNIT LOCATION

 UNIT RATING

 FUEL CHARACTERISTICS

 FGD VENDOR

 PROCESS

 NEW OR RETROFIT

 START UP  DATE

 FGD STATUS

 EFFICIENCY,
   PARTICULATES
 KANSAS  CITY  POWER  &  LIGHT

 HAWTHORN  NO.  3

 KANSAS  CITY   MISSOURI

  140  MW

 COAL    0.5-3.b  PERCENT  SULFUR

 COMBUSTION  ENGINEERING

 LIME  SCRUBBING

 RETROFIT

 11/72

 OPERATIONAL


 99 PERCENT
   soe
                        70  PERCENT
  WATER  MAKE  UP
 OPEN LOOP 7.0 GPM/MW
  SLUDGE  DISPOSAL
 PLANT SITE DISPOSAL POND
  UNIT COST
SEE APPENDIX A,  FSD SYSTEM ECONOMICS
  OPERATIONAL
   EXPERIENCE
 REFER TO THE BACKGROUND INFORMATION SECTION IN TABLE  3 OF  THIS  REPORT.
 THE SCRUBBER PLANT HAS BEEN CONVERTED FROM A  LIMESTONE FURNACE  INJECTION
 AND TAIL-END SCRUBBING SYSTEM TO A TAIL-END WET LIME  SCRUBBING  SYSTEM.
 LIME-BASED OPERATIONS COMMENCED ON FEBRUARY 7,  1977.  COMPLIANCE TESTING
 FOR KANSAS CITY PARTICULATE STANDARDS INDICATED THE  NO.3  UNIT WAS  WELL
 WITHIN THE 0.17 POUND REGULATION.  THE 3-MOOULE SCRUBBER  PLANT CAN  ONLY BE
 BY-PASSED DURING EMERGENCIES.
                                               45

-------
                                       BACKGROUND INFORMATION
                                                 ON
                                        HAWTHORN NOS. 3 AND 4

     THE HAWTHORN POWER STATION IS OWNED AND OPERATED BY THE KANSAS CITY POWER AND LIGHT  COMPANY  AND
SITUATED IN A HEAVILY INDUSTRIALIZED AREA ON THE NORTH BANK OF THE MISSOURI RIVER IN EAST  KANSAS
CITY, MISSOURI.  THE PLANT CONTAINS FIVE COAL-FIRED BOILERS.  UNITS 1 AND 2 ARE CONSIDERED  PEAK
BOILERS, EACH RATED AT 80 MW.  UNITS 3 AND 4 ARE CYCLIC-LOAD BOILERS. EACH RATED AT 100 MW.   UNIT 5
IS A BASE-LOAD BOILER RATED AT 500 MW.  UNITS 1 TO 4 WERE PURCHASED AND PLACED IN SERVICE  BETWEEN
1950 AND 1955.  UNIT NO. 5 WAS PLACED IN SERVICE IN EARLY 1970.  ALL THE HAWTHORN BOILERS  ARE  DRY-
BOTTOM PULVERIZEO-COAL-FIRED UNITS DESIGNED AND MANUFACTURED BY COMBUSTION ENGINEERING.   TWO  GRADES
OF COAL ARE BURNED AT THE STATION; A LOW SULFUR COAL FROM THE WYOMING AREA THAT TYPICALLY  CONTAINS
0.5X SULFUR AND 11 PERCENT ASH WITH A HEATING VALUE OF 9800 8TU/LB AND A HIGH SULFUR COAL  FROM
OKLAHOMA THAT TYPICALLY CONTAINS 3.5X SULFUR AND la PERCENT ASH WITH A HEATING VALUE OF 11,500
BTU/LB.  OF THE FIVE COAL-FIRED BOILERS INSTALLED AT THE STATION, TWO UNITS 3 AND 4 HAVE  BEEN  RETRO-
FITTED WITH PARTICULATE AND SULFUR DIOXIDE SCRUBBER PLANTS.

     THE ORIGINAL SCRUBBER PLANTS INSTALLED ON UNITS 3 AND 4 CONSISTED OF LIMESTONE INJECTION  AND
TAIL-END WET SCRUBBER MODULES SUPPLIED BY COMBUSTION ENGINEERING AND PLACED IN SERVICE NOVEMBER
1973 AND AUGUST 1972, RESPECTIVELY.  A GENERAL DESCRIPTION OF THE PROCESS FOLLOWS; DRY
LIMESTONE WAS INJECTED DIRECTLY INTO THE FURNACE BOX AND CALCINED TO LIME.  THE FURNACE-CALCINED
LIMESTONE AND BOILER FLUE GAS WERE THEN DISCHARGED TO A TAIL-END WET SCRUBBING SYSTEM CONSISTING  OF
TWO MARBLE-BED ABSORBERS WHERE PARTICULATES AND SULFUR DIOXIDE WERE REMOVED FROM THE GAS  STREAM.
THE SPENT LIME AND OTHER SCRUBBING WASTES WERE THEN DISCHARGED INTO A COMMON CLARIFIER TANK AND THE
UNDERFLOW WAS PUMPED, UNTREATED AND UNSTABILIZED, TO AN UNLINED DISPOSAL POND USED FOR THE DISPOSAL
OF FLY ASH FROM THE OTHER BOILERS.  THE SCRUBBER PLANT INSTALLED ON EACH BOILER CONTAINED TWO
IDENTICAL MARBLE-BED ABSORBERS, EACH CAPABLE OF TREATING 500,000 ACFM OF FLUE GAS AT 300 F.  A
CHEVRON-TYPE MIST ELIMINATOR AND A FINNED-TUBE STEAM REHEATER WERE ALSO INCORPORATED IN EACH MODULE
IN ADDITION TO A MIST ELIMINATOR WASH SYSTEM CONSISTING OF EIGHT AUTOMATICALLY-OPERATED WATER
LANCES.  BY-PASSING OF THE MODULES WAS POSSIBLE THROUGH A SERIES OF DAMPERS AND DUCTWORK  AROUND EACH
MODULE.

     THE ORIGINAL SCRUBBER DESIGN OF THE SYSTEM INSTALLED ON THE NO. 4 BOILER HAD TO BE MODIFIED
SHORTLY AFTER START-UP BECAUSE OF BOILER TUBE PLUGGING ATTRIBUTED TO THE LIMESTONE INJECTION.  THE
MODE OF OPERATION OF THIS SYSTEM WAS MODIFIED TO LIMESTONE INJECTION INTO THE FLUE GAS DUCT NEAR THE
INLET TO THE MARBLE-BED ABSORBER.  THE SIMPLIFIED PROCESS FLOW DIAGRAMS OF THESE ORIGINAL SCRUBBEK
PLANTS ARE PRESENTED IN APPENDIX B.
                                                 46

-------
KANSAS CITY POWER & LIGHT                                        HAWTHORN UNIT NO. 3

       OPERATING HOURS                   F6D  OPEkABlLITY  (X)
MONTH       BOILER       MODULE  3A       MODULE 38    MODULE  A      MODULE B

JUL. 75      584              o              247          o             42
       PROBLEMS WITH  MODULE  3A  INCLUDED  A LEAK IN CITY  WATER LINE,  A PLUGGED DUCT TO THE 1.0.  FAN,
       A MALFUNCTIONING  OUTLET  DAMPER FROM THE SCRUBBER.  IN MODULE B MARBLES HERE LOST FROM THE
       BED AND A SPRAY HEADER WAS  BROKEN.

AUG. 75       0               0              00             0
       LOST I.D. FAN  FOR HALF OF THE BOILER.  CARRYOVER  OF JULY PROBLEMS.

SEP. 75      358            247              81          69            23
       OUTAGE DUE TO  CLEANING AND  MECHANICAL REPAIRS.  POTS, COVERS, AND MARBLES IN THE MARBLE BED
       OF  MODULE 38 WERE REPLACED.

OCT. 75      180             117             145         65            81
       MODULE 3A OUTAGE  WAS  DUE LARGELY  TO REPLACEMENT  OF A  RECYCLE PUMP MOTOK.   A SCHEDULED BOILER
       OVERHAUL  REDUCED  BOILER  OPERATION HOURS.

NOV. 75         0              0               00             0

DEC. 75         0              0               00             0

JAN. 76         0              0               00             0
       BOILERS  AND  SCRUBBERS WERE  SHUTDOWN FOR A SCHEDULED TURBINE  OVERHAUL.  THE SYSTEM IS SCHEDUL-
       ED  TO GO  BACK  ON-LINE IN JANUARY  1976.  SYSTEM WAS DOWN ALL  MONTH BECAUSE OF FROZEN EQUIP-
       MENT  AND  LINES AND  A  MANPOWER SHORTAGE DUE TO A  BOILER AND TURBINE OVERHAUL UN ANOTHER  UNIT
       AT  THIS  STATION.

FEB.  76       503           148              7          37             1
         SCRUBBER OUTAGES RESULTED  FROM PLUGGING IN THE  SCRUBBER BED, CAUSED BY CONVERSION FROM AN
         UNDER-BED  TO  OVER-BED SPRAY SYSTEM.

MAR.  76         0             0               00             0

 APR.  76         0             0               00             0
        RECONVERSION OF MODULE 36'S SPRAY SYSTEM ARRANGEMENT  HAS BEEN COMPLETED.   ALSO THE BYPASS
        SYSTEM  HAS  BEEN MODIFIED AND CHANGED TO A SLIDE-GATE  DAMPER  ARRANGEMENT.

MAY.  76         0             0               00             0
        THE SYSTEM WAS SHUT DOWN DURING THE MONTH DUE TO THE  CONTINUATION OF MANPOWER SHORTAGE
        PROBLEMS.  THE UTILITY DID  PERFORM SOME CLEANING AND  REPAIRS DURING THE MONTH.

 JUN.  76       505           198             230         39             44
        THE UTILITY  IS IN THE PROCESS OF  MODIFYING THE DEMISTER WASH SYSTEM BOTH  UNITS NOS. 3 AND 4.
        THE WATER LANCES, FORMERLY  CONSTRUCTED OF FRP, ARE BEING CHANGED TO CARBON STEEL COMPONENTS
        IN ORDER TO RECTIFY LOSS OF SPRAY NOZZLES AND SUBSEQUENT SHATTERING OF THE LANCES.

 JUL.  76

 AUG.  76
        THE UTILITY  IS NOW IN THE PROCESS OF CONVERTING THIS  SYSTEM FROM LIMESTONE INJECTION AND
        TAIL END SCRUBBING TO A LIME SLURRY BASED SCRUBBING SYSTEM.

 SEP.  76

 OCT.  76
        THE SYSTEM WAS VIRTUALLY OUT OF SERVICE THE ENTIRE REPORT PERIOD.  MANPOWER COMMITMENTS WERE
        SERIOUSLY HAMPERED BY A MAJOR EXPLOSION WHICH OCCURRED IN THE COAL MILL PULVERIZING AREA OF
        HAWTHORN NO. 5.

 NOV.  76          0             0               00              0

 DEC.  76          0             0               00              0
        THE UNIT DID NOT OPERATE DURING THE PERIOD BECAUSE OF THE ONGOING MAJOR MODIFICATIONS BEING
        IMPLEMENTED TO THE SCRUBBING SYSTEM.  THE SYSTEM SHOULD BE READY FOR OPERATION FEB. 1.  THE
        UNIT MUST UNDERGO A SERIES OF TESTS TO INSURE COMPLIANCE WITH CITY AND FEDERAL REGULATIONS.

 JAN.  77         0             0               00              0

FEB.  77       383           337             264         88             69

MAR.  77       482           476             411         99             85
        THE NO.  3 UNIT WAS DOWN THE ENTIRE MONTH OF JANUARY FOR COMPLETION UF MODIFICATIONS AND
        REPAIRS  TO THE SCRUBBERS AND BOILER.  THE UNIT BECAME AVAILABLE FOR  SERVICE AND  TESTING ON
                                                   47

-------
KANSAS CITY POWER & LIGHT                                       HAWTHORN  UNIT  NO.  3

       OPERATING HOURS                  F6D OPEKABILITY  CX)
MONTH       BOILER       MODULE 3A      MODULE 3B     MODULE  A     MODULE  B

       FEB. 7.  THE UNIT'S MEASURED PARTICULATE EMISSIONS  AT  THE SCRUBBER  OUTLET WAS  0.12  LH/MM
       BTU (WELL BELOW THE 0.17 LB REGS).  A BLEND OF APPROXIMATELY 2.0 X  SULFUK COAL IS BEING FIKEO
       IN THE BOILER.  THE CONVERSION FROM LIMESTONE TO  LIME  HAS BEEN GOOD.  SOME  INITIAL  PROBLEMS
       WITH PROCESS CHEMISTRY CONTROL HAVE BEEN CORRECTED.  IN ADDITION,  SOME  MINOR MECHANICAL
       PROBLEMS IN THE FORM OF PUMP MALFUNCTIONS AND LOSS  OF  SLAKING WATER PRESSURE HAVE BEEN
       ENCOUNTERED.  SYSTEM OPERATIONS ARE STILL CONTINUING AT OX SOLIDS  AND 100X  SLOWDOWN.   FRESH
       WATER MAKE-UP REQUIREMENT IS APPROXIMATELY 7.0 GPM/MW.

APR. 77      720           
-------
KANSAS CITY POWER & LIGHT                                        HAWTHORN  UNIT  NO.  3

                                                                 FGD  SYSTEM
MONTH     PERIOD MRS.      BOILER MRS.      FGD  SYSTEM  MRS.    AVAILABILITY  CX)

OCT. 77      744               00                    0

NOV. 77      730             411                 411                   57
       THE UNIT WAS SHUT DOWN BECAUSE OF  A  LACK  OF NATURAL GAS.  DURING THIS PERIOD THE FGD SYSTEM
       WAS OVERHAULED.  THE  ORIGINAL REACTION  TANKS  AND SPRAY  HEADERS WERE  REPLACED BY STAINLESS
       STEEL COMPONENTS.   THE INTERCONNECTING  PIPING IS RUBBER LINED. THE  UNIT BEGAN FIRING COAL
       NOVEMBER 3.
NOTES  THE BOILER AND FGD  SYSTEM MUST RUN SIMULTANEOUSLY  BECAUSE NO BY-PASS  IS ALLOWED EXCEPT DUR-
       ING EMERGENCIES.  WHENEVER THE BOILER  IS  DOWN THE  SCRUBBER  IS  EFFECTIVELY UNAVAILABLE BECAUSE
       THE DOWN TIME  IS UTILIZED FOR SCRUBBER  MAINTENANCE AND  REPAIR. THEREFORE,  AVAILABILITY AND
       UTILIZATION FACTORS ARE IDENTICAL  FOR  THIS SYSTEM.

DEC.  77        744             541              541                    73
JAN.  78         744            346              346               47
       OUTAGES SOME LEAKS  IN THE FGD PIPING WERE REPLACED AND  MODULES WERE  CLEANED.  THERE WERE
       NO  FGO  RELATED OUTAGES.
                                                    49

-------
                  TABLE 3
PERFORMANCE DESCRIPTION FOR OPERATIONAL FGD SYSTEMS THROUGH   01/78
 UTILITY NAME

 UNIT NAME

 UNIT LOCATION

 UNIT RATING

 FUEL CHARACTERISTICS

 FGD VENDOR

 PROCESS

 NEW OR RETROFIT

 START UP DATE

 FGD STATUS

 EFFICIENCY,
  PARTICULATES
 KANSAS  CITY  POWER & LIGHT

 HAWTHORN NO.  4

 KANSAS  CITY   MISSOURI

  100  MH

 COAL    0.5-3.5 PERCENT  SULFUR

 COMBUSTION  ENGINEERING

 LIME  SCRUBBING

 RETROFIT

  8/73

 OPERA-TIONAL


 99 PERCENT
  S02
                       70 PERCENT
 WATER MAKE UP
                       OPEN LOOP 7.0 GPM/MW
  SLUDGE DISPOSAL
                       PLANT SITE DISPOSAL POND
  UNIT COST
SEE APPENDIX A,  FGU SYSTEM ECONOMICS
  OPERATIONAL
   EXPERIENCE
 REFER TO THE BACKGROUND INFORMATION SECTION IN TABLE 3 OF THIS REPORT.
 THE SCRUBBER PLANT HAS BEEN CONVERTED FROM A LIMESTONE FURNACE INJECTION
 AND TAIL-END SCRUBBING SYSTEM TO A TAIL-END WET LIME SCRUBBING SYSTEM.
 OPERATIONS IN THE LIME SCRUBBING MODE COMMENCED ON JANUARY 1, 1977.
 COMPLIANCE TESTING FOR KANSAS CITY PARTICULATE REGULATIONS INDICATED THE
 UNIT IS MEETING THE 0.17 POUND REGULATION. THE 2-MODULE SCRUBBER PLANT
 CAN ONLY BE BY-PASSED DURING EMERGENCIES.
                                               50

-------
                                        BACKGROUND  INFORMATION
                                                 ON
                                         HAWTHORN NOS.  3  AND  a

     THE HAWTHORN POWER STATION  IS  OWNED  AND  OPERATED  BY  THE KANSAS  CITY  POWER  AND  LIGHT  COMPANY  AND
SITUATED IN A HEAVILY  INDUSTRIALIZED  AREA  ON  THE NORTH BANK  OF  THE MISSOURI  RIVER  IN  EAST  KANSAS
CITY, MISSOURI.  THE PLANT CONTAINS FIVE  COAL-FIRED  BOILERS.   UNITS  1  AND 2  ARE  CONSIDERED PEAK
BOILERS, EACH RATED AT «0 MW.  UNITS  3  AND  4  ARE CYCLIC-LOAD BOILERS.  EACH RATED AT 100 MW.   UNIT 5
IS A BASE-LOAD BOILER  RATED  AT 500  MW.   UNITS 1  TO 4 WERE PURCHASED  AND  PLACED  IN  SERVICE  BETWEEN
1950 AND 1955.  UNIT NO. 5 WAS PLACED  IN  SERVICE IN  EARLY 1970.   ALL THE  HAWTHORN  BOILERS  ARE DRY-
BOTTOM PULVERIZED-COAL-FIRED  UNITS  DESIGNED  AND  MANUFACTURED BY  COMBUSTION ENGINEERING.   TWO  GRADES
OF COAL ARE BURNED AT  THE STATION:  A  LOW  SULFUR  COAL FROM THE  WYOMING  AREA THAT  TYPICALLY  CONTAINS
0.5X SULFUR AND 11 PERCENT ASH WITH A  HEATING VALUE  OF 9800  BTU/LB AND A  HIGH  SULFUR  COAL  FROM
OKLAHOMA THAT TYPICALLY CONTAINS 3.5X  SULFUR  AND 14  PERCENT  ASH  WITH A HEATING  VALUE  OF 11,500
BTU/LB. OF THE FIVE COAL-FIRED BOILERS  INSTALLED AT  THE  STATION,  UNITS 3  AND 4  HAVE BEEN  RETRO-
FITTED WITH PARTICULATE AND  SULFUR  DIOXIDE  SCRUB8ER  PLANTS.

     THE ORIGINAL SCRUBBER PLANTS INSTALLED  ON UNITS 3 AND 4 CONSISTED OF LIMESTONE INJECTION AND
TAIL-END WET  SCRUBBER  MODULES SUPPLIED  BY  COMBUSTION ENGINEERING  AND PLACED  IN  SERVICE NOVEMBER
1972 AND AUGUST 1972,  RESPECTIVELY.   A  GENERAL PROCESS DESCRIPTION OF  THE PROCESS  FOLLOWS:  DRY
LIMESTONE  WAS INJECTED DIRECTLY  INTO  THE  FURNACE BOX AND  CALCINED TO LIME.  THE  FURNACE-CALCINED
LIMESTONE  AND BOILER FLUE GAS WERE  THEN DISCHARGED TO  A  TAIL-END  WET SCRUBBING  SYSTEM CONSISTING  OF
TWO  MARBLE-BED ABSORBERS WHERE PARTICULATES  AND  SULFUR DIOXIDE  WERE  REMOVED  FROM THE  GAS  STREAM.
THE  SPENT  LIME AND OTHER SCRUBBING  WASTES  WERE THEN  DISCHARGED  INTO  A  COMMON CLARIFIER TANK AND THE
UNDERFLOW  WAS PUMPED,  UNTREATED  AND UNSTABILIZED,  TO AN  UNLINED  DISPOSAL  POND  USED  FOR THE DISPOSAL
OF  FLY  ASH FROM THE OTHER BOILERS.  THE SCRUBBER PLANT INSTALLED ON  EACH  BOILER  CONTAINED  TWO
IDENTICAL  MARBLE-BED ABSORBERS,  EACH  CAPABLE  OF  TREATING  500,000  ACFM  OF  FLUE  GAS  AT  300  F.   A
CHEVRON-TYPE  MIST ELIMINATOR AND A  FINNED-TUBE STEAM REHEATER  WERE ALSO  INCORPORATED  IN EACH  MODULE
IN  ADDITION  TO A  MIST  ELIMINATOR WASH SYSTEM CONSISTING  OF EIGHT  AUTOMATICALLY-OPERATED WATER
LANCES.  BY-PASSING OF THE MODULES  WAS POSSIBLE  THROUGH  A SERIES  OF  DAMPERS  AND  DUCTWORK  AROUND EACH
MODULE.

      THE ORIGINAL SCRUBBER DESIGN OF  THE SYSTEM INSTALLED ON THE  NO. 4 BOILER  HAD  TO  BE MODIFIED
SHORTLY  AFTER START-UP BECAUSE  OF BOILER TUBE PLUGGING ATTRIBUTED TO THE  LIMESTONE  INJECTION.  THE
MODE OF  OPERATION OF  THIS  SYSTEM WAS  MODIFIED TO LIMESTONE INJECTION INTO THE  FLUE  GAS DUCT NEAR  THE
 INLET  TO  THE  MARBLE-BED  ABSORBER.  THE SIMPLIFIED  PROCESS FLOW  DIAGRAMS  OF THESE ORIGINAL  SCRUBBER
PLANTS ARE PRESENTED  IN  APPENDIX B.
                                                    51

-------
KANSAS CITY POWER & LIGHT
                                                                 HAWTHORN  UNIT  NO.  4
MONTH
    OPERATING HOURS
BOILER        MODULE 4A
                                            MODULE 4B
                                   FGD OPERABILITY  (X)
                                MODULE A        MODULE B
JUL. 75       518              41              128                8               25
       MARBLE BED PLUGGING AND STRAINER PROBLEMS ON BOTH MODULES.

AUG. 75                       168              212
       LOST HALF OF BOILER DUE TO NO. 4B I.D. FAN OUTAGE.  BOTH FGD MODULES  WERE  SHUT  DOWN  TO ENSURE
       AGAINST THE LOSS OF THE ENTIRE UNIT.  NEW CHEMISTRY- ATTEMPTING TO RUN AT  IOOX  SLOWDOWN AND
       NEAR ZERO PERCENT SOLIDS.  EMPHASIS ON PARTICULATE CONTROL.  MAINTAINING PH AT  5  WITHOUT
       LIMESTONE INJECTION.

SEP. 75      395             206               210               52               53
       SCRUBBER MODULES WERE RETURNED TO SERVICE ON SEP. 21 AFTER REPLACEMENT OF  THE ORIGINAL I.D.
       FAN ON MODULE 48 SIDE.
       NEW PROCESS DESIGN - MARBLES REMOVED FROM SCRUBBER BED OF MODULE A AND REPLACED WITH A STAIN-
       LESS STEEL PERFORATED BED.  THE MARBLES WERE REMOVED BECAUSE OF CONTINUING OPERATIONAL
       DIFFICULTIES.  VERY GOOD PERFORMANCE RESULTED IN INCREASED AVAILABILITY AND CONTINUATION OF
       HIGH PARTICULATE REMOVAL EFFICIENCY C97 PERCENT).

OCT. 75      721             429               656               60               91
       MINOR BOILER RESTRICTION ON THE MODULE 4A SIDE BETWEEN THE ECONOMIZER AND  THE INLET  DRAFT
       DUCT-CHEMISTRY PROCESS MODIFICATION OF RUNNING AT 100 PERCENT BLOWDOWN AND ZERO PERCENT
       SOLIDS IS STILL  IN PROGRESS.  S02 REMOVAL EFFICIENCY IN THE 50 TO 60  PERCENT RANGE.   KCP&L
       IS CONCENTRATING HEAVILY ON PARTICULATE EMISSION CONTROL.

NOV. 75      720               0               713                0               99
       MODULE 4A WAS SHUT DOWN DURING THE REPORT PERIOD BECAUSE OF LOSS OF DRAFT  THROUGH  THE DUCT-
       WORK FROM THE ECONOMIZER TO THE AIR PREHEATER.  THE REHEATER PLUGGED  FREQUENTLY UNTIL THE
       SYSTEM WAS SHUT  DOWN.
DEC. 75
              640
                                               103
                                                                                  16
       BOILER OUTAGE OF 5 DAYS WAS DUE TO A SCHEDULED OVERHAUL.
JAN. 76         0               0                0                0               0
       THE SYSTEM WAS DOWN ALL MONTH BECAUSE OF FROZEN EQUIPMENT AND LINES; MANPOWER WAS  ASSIGNED
       TO A BOILER AND TURBINE OVERHAUL ON ANOTHER UNIT.

FEB. 76       579               0              450                0              78
       MODULE 4A WAS SHUT DOWN THE ENTIRE MONTH BECAUSE OF CONTINUING LOSS OF DRAFT THROUGH  THE
       DUCTWORK FROM THE ECONOMIZER TO THE AIR PREHEATER.  MARBLE BED PLUGGING AND LOSS OF A  RECYCLE
       PUMP OCCUREO ON MODULE 4B.
MAR. 76
APR. 76
 706
 550
  0
231
 24
220
 0
42
 3
40
       DURING  THE REPORT PERIOD THE UNIT'S BYPASS SEALS WERE REPLACED WITH SLIDE-GATE DAMPERS.

 MAY   76        365              99               99               27              27
 JUN.  76        460             294               23               65               5
       EXPERIENCING PLUGGING PROBLEMS.  ONE SECTION OF THE REHEAT TUBE BUNDLES HAS BEEN  REMOVED  IN
       ORDER TO FACILITATE CLEANING AND MAINTENANCE.  CURRENTLY, THE UTILITY IS  IN THE PROCESS OF
       MODIFYING THE SCRUBBING SYSTEM FHOM A LIMESTONE INJECTION AND TAIL-END BASED SYSTEM  TO A
       LIME SLURRY-BASED SYSTEM.
 SEP. 76
 OCT. 76
       THE SYSTEM WAS OUT OF SERVICE VIRTUALLY THE ENTIRE REPORT PERIOD.  OPERATIONS AND MANPOWER
       COMMITMENTS WERE SERIOUSLY HAMPERED BY A MAJOR EXPLOSION WHICH OCCURRED  IN THE COAL  MILL  PUL-
       VERIZING AREA OF HAWTHORN NO. 5.
NOV. 76
DEC. 76
 786
   0
442
  0
                  91
                   0
       THE UTILITY IS IN THE PROCESS OF CONVERTING THE SYSTEM TO A WET-LIME SCRUBBING  SYSTEM.
       START-UP IN THE LIME SCRUBBING MODE WILL COMMENCE THE FIRST PART OF JANUARY.
JAN. 77
FEB. 77
MAR. 77
 572
 591
 539
486
168
440
424
292
525
 85
80
97
 74
50
82
       THE UNIT BECAME AVAILABLE FOR SERVICE IN THE LIME SCRUBBING MODE ON JAN.  1,  1977.   TESTING
       FOR COMPLIANCE WITH PARTICULATE CODES OCCURRED DURING THE MONTH.  THE 0.17 LB/MM BTU  EMISSION
       REGULATION IS BEING MET BY THE NO. 4 UNIT.  A BLEND OF APPROXIMATELY 2.OX SULFUR COAL IS
       BEING BURNED IN THE UNIT TO REMEDY THIS.  SOME REHEAT PROBLEMS AND PLUGGING  IN  THE  SUCTION
       OF THE RECYCLE TANK BY A RAINCOAT WERE ALSO REPORTED.  SYSTEM OPERATIONS  ARE  STILL  CONTINUING
       AT OX SOLIDS AND 100X BLOWDOWN.  THE FRESH WATER MAKE-UP REQUIREMENT IS 7.0  GPM/MW.

-------
KANSAS CITY POWER & LIGHT                                         HAWTHORN UNIT NO.  4

                 OPERATING  HOURS                                  F60 OPERABILITY  (Z)
MONTH        BOILER         MODULE  4A         MODULE 48         MODULE A        MODULE B

APR. 77       720              311               311               43              43
MAY  77       740              180               180               54              54
       THE SYSTEM IS  NOW  OPERATING WELL  AT  ABOUT  15-25X SLOWDOWN.  THE PH CONTROL SYSTEM OPERATIONS
       HAVE BEEN EXCELLENT.   DURING MAY  THE BOILER BURNED GAS FOR 408 HOURS.   THE OPERABILITY  VALUES
       00 NOT INCLUDE THESE  HOURS.  THE  OPERABILITY VALUES DO NOT INCLUDE THESE HOURS.  S02  REMOVAL
       EFFICIENCY IS  ESTIMATED AT  50-60* FOR BOTH A AND B SCRUBBING MODULES,  ALTHOUGH ACTUAL TESTS
       HAVE NOT BEEN  RUN  FOR ABOUT ONI-ANO-A-HALF YEARS.  CURRENTLY BOTH MODULES  ARE BEING  OPERATED
SIMULTANEOUSLY.

JUN. 77       720     FGD  NOT REQUIRED-NATURAL GAS
       UNIT NO. 4 FIRED GAS THROUGHOUT  THE  MONTH.  THE SCRUBBER PLANT WAS SHUT DOWN FOR  MODIFICA-
       TIONS DURING  THE PERIOD.   SPECIFICALLY,  ALL THE INTERNAL SCRUBBER COMPONENTS WERE REPLACED
       WITH 316 LSS  (UNDER-BED SPRAY  HEADERS),  A  NEW REACTION TANK LINER WAS  INSTALLED,  AND  RUBBER-
       LINED PIPING  REPLACED THE  ORIGINAL CARBON  STEEL RECYCLE PIPING (FROM THE RECYCLE  PUMPS  TO
       THE SPRAY MAIIFOLD).

JUL. 77       696              120               120
       THE STAINLESS  STEEL  MODIFICATIONS WERE COMPLETED BY JULY 25 AND THE UNIT RESUMED  COAL FIRING.
       THE SCRUBBER  MODULES WERE  IN SERVICE APPROXIMATELY ISO HOURS FOR THE REMAINDER OF THE MONTH.
       THE SYSTEM SUCCESSFULLY COMPLETED FEDERAL  PARTICULATE REMOVAL TESTS (0.15  LB/MM BTU  MEASURED)
       DURING THIS  TIME.   THE UNIT FIRED THE HIGH SULFUR, HIGH ASH (PEABODY-OKLAHOMA) COAL  DURING
       THE TEST.  OPACITY TESTS FOR BOTH UNITS 3  AND 4 WILL BE CONDUCTED IN SEPTEMBER.

AUG.  77       550              550               550              74              74
SEP.  77       589              520               520              73              73
       DURING THE LATTER  PART OF  SEPTEMBER  THE CLARIFIER BECAME PLUGGED.  THE UNIT  FIRED NATURAL
       GAS WHILE  THE CLARIFIER WAS CLEANED.
                                                   53

-------
KANSAS CITY POWER & LIGHT                                       HAWTHORN UNIT NO. t

                                                                                FGD SYSTEM
MONTH         PERIOD HRS.     BOILER HRS.          FGD SYSTEM HRS.              AVAILABILITY  (*J

OCT. 77          744            550                      550                          7a
NOV. 77          780            496                      496                          *><*
       A GENERATOR EXCITER PROBLEM CAUSED A BOILER OUTAGE DURING OCTOBER.  THERE WERE TWO OTHER
       OUTAGES DURING OCTOBER THAT WERE SCRUBBER RELATED.  THE FIRST WAS CAUSED BY A PLUGGED  HEADER
       AND THE SECOND OCCURRED WHEN THE LIQUID LEVEL IN INTERNAL REACTION TANK EXCEEDED CONTROL
       LEVEL RESULTING IN PROBLEMS TO THE INLET GAS DUCT OG THE SCRUBBER.  DURING NOVEMBER  THERE
       WERE TWO INSTANCES OF PLUGGED UNDER BED NOZZLES ON THE 4A MODULE.  THE SCRUBBER WAS  DOWN
       U7.33 HOURS FOR FGD RELATED MAINTENANCE.
       ON NOVEMBER 10 AN EPA OPACITY TEST WAS RUN ON MODULES 3 AND 4.  AVERAGE OPACITY WAS  16.76X
       RUNNING AT OR NEAR FULL LOAD.  THE UNITS ARE NOW CERTIFIED FOR PARTICULATE AND OPACITY.

NOTE:  THE BOILER AND FGD SYSTEM MUST RUN SIMULTANEOUSLY BECAUSE NO BY-PASS IS ALLOWED EXCEPT DURING
       EMERGENCIES.  WHENEVER THE BOILER IS DOWN THE SCRUBBER IS EFFECTIVELY UNAVAILABLE BECAUSE
       THE DOWN TIME IS UTILIZED FOR SCRUBBER MAINTENANCE AND REPAIR.  THREEFOREi AVAILABILITY AND
       UTILIZATION FACTORS ARE IDENTICAL FOR THIS SYSTEM.

DEC. 77        744            530                        520                    70
JAN. 78        744            508                        508                    68
       MODULE 4A HAD SEVERAL PROBLEMS INCLUDING SPRAY NOZZLE PLUGGING.  THE SCRUBBER ON THE RECYCLE
       PUMP MALFUNCTIONED.  SOME NEW SPRAY NOZZLES WERE INSTALLED.  THERE WERE SEVERAL BOILER
       RELATED OUTAGES.
                                                  54

-------
                  TABLE  3
PERFORMANCE DESCRIPTION  FOR  OPERATIONAL  FGD  SYSTEMS  THROUGH   01/78
 UTILITY NAME

 UNIT NAME

 UNIT LOCATION

 UNIT RATING

 FUEL CHARACTERISTICS

 FGD VENDOR

 PROCESS

 NEW OR RETROFIT

 START UP  DATE

 FGD STATUS

 EFFICIENCY,
   PARTICULATES
 KANSAS  CITY  POWER & LIGHT

 LA  CYGNE  NO  1

 LA  CYGNE  KANSAS

  820  MW

 COAL  5.0  PERCENT  SULFUR

 BABCOCK & WILCOX

 LIMESTONE SCRUBBING

 NEW

  2/73

 OPERATIONAL


 98  PERCENT
   S02
                        76 PERCENT
  WATER  MAKE  UP
                        OPEN LOOP 1.4 SPM/MW
  SLUDGE DISPOSAL
 PLANT SITE DISPOSAL POND
  UNIT  COST
SEE APPENDIX A, FGD SYSTEM ECONOMICS
  OPERATIONAL
   EXPERIENCE
 REFER TO THE BACKGROUND INFORMATION SECTION IN TABLE 3 OF THIS REPORT.
 THE EMISSION CONTROL SYSTEM FOR THIS NEW COAL-FIRED POWER-GENERATING UNIT
 CONSISTS OF EIGHT SCRUBBER MODULES FOH FLY ASH AND 302 REMOVAL. EACH
 MODULE INCLUDES A VENTURI SCRUBBER IN SERIES WITH A 2-STAGE IMPINGEMENT
 PLATE ABSORBER.  THE SCRUBBER PLANT is AN INTEGRAL PART OF THE POWER-
 GENERATING COMPLEX, ALLOWING NO FLUE GAS BYPASS.   INITIAL OPERATIONS
 COMMENCED IN FEB. 1973. COMMERCIAL SERVICE WAS ATTAINED BY JUNE 1973.
 TOTAL SYSTEM AVAILABILITY FOR THE MONTH OF JANUARY WAS 9« PERCENT.
                                                55

-------
                                       BACKGROUND INFORMATION
                                                 ON
                                        LA CYGNt UNIT NO. 1

     THE LA CYGNE POWER STATION OF KANSAS CITY POWER AND LIGHT COMPANY BEGAN COMMERCIAL  OPERATION ON
JUNE 1,  1973, AS A JOINT PROJECT OF KANSAS GAS AND ELECTRIC COMPANY AND KANSAS  CITY  POWER  *  LIGHT
COMPANY.  THE STATION IS LOCATED ABOUT 55 MILES SOUTH OF KANSAS CITY, IN LINN COUNTY,  KANSAS.

     ELECTRIC POWER GENERATING FACILITY CONSISTS OF TWO COAL-FIRED BASE-LOAD BOILERS  WITH  ASSOCIATED
STEAM TURBINES AND ELECTRIC GENERATORS.  THE PLANT HAS THREE OIL-FIRED BOILERS, USED  PRIMARILY  FOR
STARTUP OF THE LARGE UNIT.  THE COMBINED IvET GENERATING CAPACITY OF THE PLANT IS  APPROXIMATELY  1450
MW (UNIT NO. 1 - 620 MW, UNIT NO. 2 - 630 MvO.

     BOILER NO. 1 AT LA CYGNE, DESIGNED BY BABCOCK AND WILCOX, IS A DRY-BOTTOM, PULVERIZED-COAL-
FIRED CYCLONE UNIT.  THE COAL BURNED IS LOW-GRADE, SUBBITUMINOUS, WITH AN AS-FIRED HEATING  VALUE OF
9000 TO 9700 BTU/LB AND ASH SULFUR CONTENTS OF £5 PERCENT AND 5 PERCENT, RESPECTIVELY.   POLLUTION
CONTROL EQUIPMENT ON THIS BOILER CONSISTS OF EIGHT SCRUBBING MODULES FOR THE CONTROL  OF  PARTICULATE
AND SULFUR DIOXIDE EMISSIONS.  THIS SCRUBBING SYSTEM WAS DESIGNED AND CONSTRUCTED BY  BABCOCK  AND
WILCOX AS AN INTEGRAL PART OF THE POWER GENERATING FACILITIES.  BYPASSING OF THE  BOILER'S  FLUE  6AS
AROUNU THE FGD SYSTEM IS NOT POSSIBLE.  A PROCESS FLOW DIAGRAM OF THE LA CYGNE  AIR QUALITY  CONTROL
SYSTEM AND RELATED MAJOR EQUIPMENT IS PRESENTED IN APPENDIX B.

PROBLEMS AND SOLUTUIONS

     THE FGD INSTALLATION HAS BEEN PLAGUED WITH NUMEROUS PROBLEMS SINCE THE FIRST TRIAL  OPERATION ON
DECEMBER 26, 1972.  SOME OF THESE PROBLEMS, SUCH AS VIBRATIONS OF THE INDUCED-DRAFT  FANS AND  THEIR
SENSITIVITY TO IMBALANCE, OCCURRED EVEN BEFORE THE BOILER WAS FIRED.  AS THESE  FABRICATION  PROBLEMS
WERE CORRECTED AND THE FGO SYSTEM WENT INTO OPERATION, TWO OTHER TYPES OF PROBLEMS APPEARED.  THE
FIRST TYPE, ASSOCIATED WITH THE WET LIMESTONE PROCESS, INCLUDED PLUGGING OF THE DEMISTER AND  STRAIN-
ERS.  THE CORROSION ASSOCIATED WITH CONDENSATION OF ACID VAPORS FROM THE GAS ON THE  REHEATER  TUBE
BUNDLES WAS CONTROLLED BY INJECTION OF SLIP STREAMS OF HOT AIR FROM THE BOILER'S  COMBUSTION  AIR
HEATER  INTO THE SCRUBBED FLUE GASES AT THE INLET TO THE REHEATER UNITS.  THIS PRACTICE,  WHICH RE-
DUCED THE MAXIMUM GENERATING CAPACITY OF THE BOILER BY LIMITING THE AIR AVAILABLE FOR  COAL COM-
BUSTION, IS NO LONGER NECESSARY BECAUSE OF RECENT SYSTEM DESIGN MODIFICATIONS.

     BECAUSE THE FGD SYSTEM INCLUDES NO SPARE MODULES AND IT CANNOT BE BYPASSED,  OUTPUT  OF  THE
BOILER  IS TOTALLY CONTROLLED BY PERFORMANCE AND AVAILABILITY OF THE FGO MODULES.  PRESENT  PROCEDURES
CALL FOR CLEANING ONE MODULE EACH NIGHT ON A ROTATIONAL SCHEDULE AND KEEPING ALL  MODULES AVAILABLE
DURING THE DAYTIME PEAK PERIODS.  CLEANUUTS REQUIRE THREE MEN FOR A PERIOD OF 10  TO  12 HOURS.
RECENT MODIFICATIONS BY THE UTILITY ON THE SCRUBBER INSTALLATION HAVE RESULTED  IN PLANS  FOR PROLONG-
ED OPERATIONAL PERIODS, WITH MODULES STAYING ON-LINE CONTINUOUSLY FOR PERIODS UP  TO  3  WEEKS.  THIS
PREVENTIVE MAINTENANCE AND CLEANOUT SCHEDULE HAS, TO DATE, NOT YET BEEN ADOPTED.

     THE UTILITY HAS RECENTLY COMPLETED ADDITIONAL SYSTEM MODIFICATIONS, INCLUDING THE INSTALLATION
OF AN EIGHTH SCRUBBING MODULE (PLACED IN COMMERCIAL SERVICE JULY 1977).  THE COST OF  THE ADDITIONAL
MODULE WAS APPROXIMATELY $5.2 MILLION AND ENABLES THE PLANT TO INCREASE ITS MAXIMUM CQNTINOUS GENER-
ATING CAPACITY FROM THE PREVIOUS 700-MW LEVEL TO 800 MW. THE ORIGINAL AIR QUALITY CONTROL  SYSTEM
DESIGN ALLOTTED ADDITIONAL SPACE FOR SUCH A SYSTEM EXPANSION.  UTHER SYSTEM MODIFICATIONS
INCLUDE:  CHANGING THE i.o. FANS IN ORDER TO MINIMIZE OR ELIMINATE A FAN PARALLELING  PROBLEM,
INSTALLATION OF ADDITIONAL BANKS OF STEAM TUBE REHEATERS, CHANGING THE MIST ELIMINATOR WASH SYSTEM,
INSTALLATION OF AN ADDITIONAL SLUDGE POND, AND IMPROVEMENT OF THE SYSTEM'S INSTRUMENTATION/CONTROL
LOOPS FOR AUTOMATIC OPERATION.
TABLE THAT FOLLOWS.
                                                  56

-------
KANSAS CITY POWER t LIGHT               OPERATING HISTORY        LA CYGNE UNIT  NO.  1
MONTH
JAN.
FEB.
MAR.
APR.
MAY
JUN.
JUL.
AUG.
SEP.
OCT.
NOV.
DEC.

74
74
74
74
74
74
74
74
74
74
74
74
BOILER HOURS












A
49
66

67
69
93
75
90
69
90
90

B
32
66

70
83
84
80
90
88
71
71

"T"*fc.r^w/i
C
44
59
BOILER
75
78
83
80
73
73
60
60
BOILER
u A i • a i rt\j
0
87
76
SHUTDOWN
88
85
90
81
81
76
61
61
SHUTDOWN
NOTE: THE 1971 FIGURES ARE BASED UPON ACTUAL SYSTEM
BOILER HOURS.
JAN.
FEB.
MAR.
APR.
MAY
JUN.
JUL.
AUG.
SEP.
OCT.
NOV.
DEC.
JAN.
FEB.
MAR.
75
75
75
75
75
75
75
75
75
75
75
75
76
76
76


694


82
5
DURING REDUCED LOAD CONDITIONS
ALTHOUGH THEY WERE AVAILABLE.
FIGURES INDICATE. 1975 FIGURES
IN THE PERIOD.
683
667
590
630
MODULES A AND D ARE
CLEANING.
610
SYSTEM SHUTDOWN OCT.
REMAINED INOPERATIVE
231
346
95
88
78


96
BOILER
BOILER
90
SHUTDOWN
SHUTDOWN
76
t/Ukt
E
23
52

74
78
82
65
81
83
84
84

OPERATION


93
F
37
100

100
84
83
79
78
69
85
85

HOURS


92
DAYS OF OPERATION
SOME OF THE MODULES WERE NOT REQUIRED
AVAILABILITY WAS THEREFORE HIGHER THAN
ARE BASED UPON SYSTEM AVAILABLE HOURS
85
85
90
94
64
90
75 88 87
USED FOR RESEARCH TESTS
78 84
16, 1975 OWING
THROUGHOUT THE
66
93
77
90
90
65
84
90
84
85
89
86
87
78 92 85
. ONE MODULE IS SHUT DOWN
84 85
TO PROBLEMS WITH
MONTH.
46
60
74
93
79
GENERATOR
72
96
78
AND I.
73
89
G AVERAGE
81
65

88
80
87
77
99
86
84
84

AS A FUNCTION


96
50
69

80
80
86
80
85
81
76
76

OF ACTUAL


90
AND THEREFORE SHUT DOWN,
SOME OF THE POSTED
AS A FUNCTION OF HOURS
83
89
85
83
EACH EVENING
74
D. AIR FAN.
65
94
89
86
66
84
FOR
60
SYSTEM
66
91
597 91 87 81 85 87 89 84 86
AVAILABILITY FIGURES FOR OCTOBER AND NOVEMBER DO NOT INCLUDE THE OUTAGE TIME FROM OCTOBER 16
TO NOVEMBER 13. BOILER OUTAGES OF 80, 50, AND 11 HOURS, TOTALING 141 HOURS, OCCURRED DURING
DECEMBER.
618
594
643
86
94
92
85
90
90
91
66
88
72
91
93
64
92
94
52
93
91
84
95
91
03
92
91
                                                   57

-------
KANSAS CITY POWER & LIGHT
                                        OPERATING HISTORY
                                                            LA CYGNE UNIT NO. 1
MONTH
           BOILER HOURS
                                  PERCENT AVAILABILITY-8Y MODULE
                                       B       C       D       E
                                                                                 AVERAGE
APR. 76                                    BOILER OVERHAUL
       THE SYSTEM WAS SHUT DOWN ON APRIL 6 FOR A SCHEDULED BOILER, AIR PREHEATER,  AND  STACK  BREECH-
       ING OVERHAUL.  DURING THIS OUTAGE SOME MAINTENANCE WAS PERFORMED ON  THE  SCRUBBER  DUCTWORK,
       PRIMARILY BECAUSE OF CORROSION PROBLEMS.

MAY  76           436          96      92      93       96      89     95     96          9"
       THE SCHEDULED UNIT OUTAGE ENDED MAY 10 WHEN THE SYSTEM WAS RESTARTED.  DURING THE  REMAINDER
       OF THE MONTH FOUR UNIT OUTAGES WERE ENCOUNTERED, TOTALING OVER 70 HOURS.
JUN. 76
                               93
                                  91      94       95      93     93     91         93
  FOUR FORCED MINOR SCRUBBER OUTAGES OCCURRED DURING THE MONTH,  RESULTING IN A TOTAL AVERAGE
  SYSTEM AVAILABILITY OF  93.33 PERCENT.
JUL.
76                        96      95      92       93      93     94     94         94
  THE UNIT RECORDED ITS LARGEST MW-HOUR MONTH SINCE INITIATION OF COMMERCIAL OPERATION.
  MINOR SCRUBBER OUTAGES OCCURRED DURING THE MONTH.
                                                                                               TWO
AUG. 76




SEP. 76

OCT. 76





NOV. 76

DEC. 76
       C
       (
       (

JAN. 77

FEB. 77

MAR. 77
                          94      93      92       94      92     90     88         92
  THE SYSTEM WAS TAKEN OUT OF  SERVICE AUGUST 24 FOR REPAIR OF A TURBINE BLADE.  THE UTILITY
  TOOK ADVANTAGE OF THIS OUTAGE PERIOD TO PROCEED WITH COATING THE STACK INNER STRUCTURE WITH
  PLASTITE 4005.  THE AUGUST AVAILABILITY FIGURES DO NOT INCLUDE THIS OUTAGE TIME.

                                      TURBINE REPAIR

                                      TURBINE REPAIR
  UNIT NO. i REMAINED OUT OF SERVICE ALL OF SEPTEMBER AND THE FIRST THREE WEEKS OF OCTOBER
  BECAUSE OF COMPLETION TO TURBINE BLADE REPAIRS WHICH COMMENCED ON AUGUST 24.  THE SYSTEM WAS
  RETURNED TO SERVICE ON OCTOBER 20.  OPERATION WAS INTERMITTENT PENDING TURBINE BLADE RE-
  BALANCING AND REESTABLISHMENT OF NORMAL OPERATING CONDITIONS.
             627
             706
                          95
                          87
                                  93
                                  89
                                          94
                                                   95
                                                   94
                                                           94
                                                           94
                                                                  93
                                                                  95
                                                                         94
                                                                         91
                                                                                    94
                                                                                    90
  DURING THE MONTH OF DECEMBER THE UTILITY  CONDUCTED SOME MINOR REPAIR AND MODIFICATION WORK
  ON THE AOCS.  SPECIFICALLY A-MOOULE EXPERIENCED SOME VENTURI  RECYCLE PUMP PROBLEMS AND THE
  c-MoouLE's REHEAT STEAM TUBE BUNDLES WERE INCREASED IN NUMBER FROM FOUR TO EIGHT.
             714

             634
94

93
                                       90

                                       93
95

93
95

94
95

93
92

94
90

88
93

93
                               94      92      86       94      91     94     90          92
       KCP&L REPORTS THAT THE 8TH MODULE HAS BEtN INSTALLED AND WILL BE PLACED IN SERVICE  SOMETIME
       DURING THE MONTH OF APRIL.  THE SYSTEM MODIFICATIONS PROGRAM IS STILL IN PROGRESS.   TWO
       CRUCIAL MODIFICATION AREAS ARE REHEAT AND MIST ELIMINATION.  ADDITIONAL BANKS OF STEAM TUBE
       BUNDLES HAVE BEEN INSTALLED IN SOME MODULES.  THE MIST ELIMINATORS IN TWO MODULES  HAVE BEEN
       MODIFIED TO THE POINT WHERE THEY HAVE BEEN OPERATING CONTINUOUSLY CLEAN.  THE AUCS'S WATER
       LOOP IS NOW 95X CLOSED.  ALSO, A NEW SETTLING POND IS BEING INSTALLED AT THE PLANT.  THE
       PLANT IS STILL GENERATING 700-720 MW DURING THE DAY AND 500-570 MW AT NIGHT.  50F  OF REHEAT
       HAS BEEN DETERMINED AS THE NECESSARY AMOUNT FOR THE LA CYNGE NO. 1 UNIT.
APR. 77
                               96
                                       94
                                                        94
                                                                       96
                                                                                         95
                                                          TURBINE PROBLEMS.
                                                        WHEN IT  IS EXPECTED
                                                                                  THE BOILER
                                                              THE
                                                              THE
                                                              AND
                                                                                 THAT 800 MW  WILL
MAY  77                                    TURBINE REPAIR
       DURING APRIL,  THE AVERAGE AVAILABILITY  INDEX FOR THE SEVEN MODULES WAS 95.2 PERCENT.
       EIGHTH MODULE  IS READY FOR OPERATION AND IN FACT HAS BEEN RUN FOR TWO DAYS.  HOWEVER,
       BOILER AND SCRUBBER SYSTEM WERE SHUT DOWN IN MAY DUE TO
       EIGHT MODULES  ARE EXPECTED TO START  UP  ABOUT JUNE 27,
       GO ON LINE.  THE MIST  ELIMINATOR WASHING CONFIGURATION IS BEING CHANGED TO WORK COUNTER-
       CURRENT TO THE GAS FLOW.   ADDITIONAL TUBE BUNDLES ARE  BEING ADDED TO INCREASE THE REHEAT
       AREA.  THESE CHANGES SHOULD BE TAKEN CARt OF BY  THE END OF JUNE.  THE NEW SETTLING POND IS
       STILL BEING DRAWN UP.   EXCAVATION HAS NOT BEGUN.

JUN. 77                                    TURBINE REPAIR
       THE UNIT REMAINED SHUT DOWN DURING THE  PERIOD AS THE TUR8HME REPAIR AND OVERHAUL CONTINUED
       MINOR CLEANOUT AND REPAIR WORK WAS DONE ON THE SCRUBBER PLANT DURING THE TURBINE OUTAGE
                                                  58

-------
KANSAS CITY POWER & LIGHT
MONTH

JUL. 77
    BOILER HOURS
      OPERATING HISTORY

PERCENT AVAILABILITY-BY MODULE
  B      C      D      E      F
                                                                  LA  CYGNE  UNIT  NO.  1
                                                                               AVERAGE
         528          95     93     94      95      95      95      95      95         95
FOLLOWING THE TURBINE OUTAGE,  THE  UNIT  WAS  PLACED  BACK  IN  COMMERCIAL  SERVICE  ON  JULY 5.
RESUMPTION OF OPERATIONS WAS CONDUCTED  WITH EIGHT  SCRUBBER MODULES  IN  THE  FLUE GAS PATH,
ENABLING THE UNIT TO OPERATE AT  A  MAXIMUM CONTINUOUS  LOAD  CAPACITY  OF  800  TO  820  Mw.   PARTI-
CULATE REMOVAL TESTS DETERMINING COMPLIANCE WITH KANSAS  REGULATIONS (0.13  LB/MM  BTU) IS
SCHEDULED TO BE CONDUCTED  IN LATE  AUGUST.
 AUG. 77

 SEP. 77
                 507
                       89
                       93
                                     94
                                           89
                                            93
                                                   90
                                                   90
                                                          93
                                                          93
                                                          95
                                                                 93
                                                                 92
                                                                               94
                                                                                         87
        THE  PARTICULATE  REMOVAL TESTS WERE CONDUCTED IN LATE AUGUST AND UNIT  NO.  1  HAS PASSED  THE
        COMPLIANCE  REQUIREMENTS.   MODULE B HAD LOW AVAILABILITY  DUE TO THE BURNING  OF  THE  MOTOR  ON
        THE  RECIRCULATING PUMP.  IT WAS REMOVED AND STARTED AGAIN AFTER 12 DAYS.
 OCT.  77
                 456
                              91
                                     96
                                           89
                                                   94
                                                          93
                                                                 94
                                                                        89
                                                                               93
                                                                                         92
        THE  SYSTEM RAN SMOOTHLY THROUGH OCTOBER,  HOWEVER,  A 12-DAY BOILER OUTAGE  WAS REQUIRED  TO  DE-
        SLAG THE BOILER.
 NOV.  77
                 234
                              93
                                     96
                                           93
                                                   94
                                                          92
                                                                 93
                                                                        96
                                                                               95
                                                                                         94
        THE BOILER HAS BEEN DOWN SINCE NOV. 15 BECAUSE OF A NECESSARY TURBINE OVERHAUL AND IS EX-
        PECTED TO GO BACK ON-LINE DEC. 19.
 DEC.  77
                300
                              98
                                    98
                                          96
                                                   96
        THE TURBINE OVEHHAUL CONTINUED UP TO DECEMBER 25.
        OUTAGES IN DECEMBER.
                                                   96       97
                                                    THERE  WERE  A
                                     98     99        97
                                     FEW SMALL BOILER RELATED
 JAN. 78
                300
                              90
                                     95
                                            95
                                                   95
                                                          93
                                                                  94
                                                                        94
                                                                               94
        THERE WERE SOME BOILER RELATED OUTAGES IN JANUARY, TOTALLING ABOUT 50 HOURS.
        CONTINUED TO OPERATE WITHOUT ANY PROBLEMS.
                                                                                   94
                                                                               THE  FGO  SYSTEM
                                                    59

-------
                  TABLE 3
PERFORMANCE DESCRIPTION FOR OPERATIONAL FGD SYSTEMS THROUGH   01/78
 UTILITY NAME

 UNIT NAME

 UNIT LOCATION

 UNIT HATING

 FUEL CHARACTERISTICS

 FGD VENDOR

 PROCESS

 NEW OR RETROFIT

 START UP DATE

 FGD STATUS

 EFFICIENCY,
  PARTICULATES
KANSAS POWER & LIGHT

LAWRENCE NO 4

LAWRENCE KANSAS

 125 MW

COAL U.5 PERCENT SULFUR

COMBUSTION ENGINEERING

LIMESTONE SCRUBBING

RETROFIT

ia/66

OPERATIONAL


99 PERCENT
  S02
                       75 PERCENT
 WATER MAKE UP
                       OPEN LOAD
 SLUDGE DISPOSAL
PLANT SITE DISPOSAL POND
 UNIT COST
 OPERATIONAL
  EXPERIENCE
REFER TO BACKGROUND INFORMATION SECTIUN IN TABLE 3 OF THIS REPORT.
THE NEW LIMESTONE FGD SYSTEM COMMENCED OPERATIONS IN EARLY JANUARY  1977.
THERE HAVE BEEN NO FORCED SCRUBBER OUTAGES REPORTED SINCE STAKT-UP.
CONTINUOUS S02 MONITORS HAVE RECORDED S02 REMOVAL EFFICIENCIES  OF BETTER
THAN B5X. PARTICULATE REMOVAL IS REPORTED TO BE EXCELLENT, YIELDING  NO
VISIBLE PLUME.  THE PLANT IS FIRING COAL RATED AT 12,300 BTU/LB  WITH A
SULFUR CONTENT OF 3.5X.
                                                60

-------
                                        BACKGROUND  INFORMATION
                                                 ON
                                            LAWRENCE NO.  4

     KANSAS POWER AND LIGHT'S LAWRENCE  NO.  4  UNIT,  AT  LAWRENCE,  KANSAS,  IS A CYCLIC-LOAD BOILER
EQUIPPED TO BURN COAL, NATURAL GAS  SUPPLEMENTED  WITH FUEL OIL,  OR A COMBINATION OF THESE THREE
FUELS.  THIS 125-MW COMBUSTION ENGINEERING  UNIT  BEGAN  GENERATING OPERATIONS IN 1959.  THE COAL FIRED
IS FROM A LOW-SULFUR SOUTHEAST WYOMING  SEAM,  AND HAS AN  AVERAGE HEATING  VALUE OF 10,000 8TU/LB, A
SULFUR CONTENT OF 0.5 PERCENT, AND  AN ASH CONTENT  OF 11  PERCENT,

     LAWRENCE NO. 4 IS NOW OPERATING WITH A RETROFITTED  COMBUSTION ENGINEERING WET LIMESTONE FGD
SYSTEM WHICH BEGAN COMMERCIAL OPERATION IN  EARLY JANUARY 1977.   THE WET  LIMESTONE SCRUBBING MODE RE-
PLACES THE ORIGINAL FGD  APPROACH  WHICH  WAS  LIMESTONE INJECTION  INTO THE  BOILER BOX FOLLOWED BY
SINGLE-STAGE MARBLE BED  SCRUBBERS.   A SIMILAR CONVERSION PROCESS IS PRESENTLY UNDERWAY AT THE 400-MW
LAWRENCE NO. 5 UNIT, CURRENTLY SCHEDULED FOR  START-UP  IN THE FIHST HALF  OF 1978.  THE FGO SYSTEMS ON
THESE TWO UNITS WILL SHARE THE NEW  WET  LIMESTONE MILLING FACILITIES AND  RECIRCULATION TANKS IN BOTH
THE PARTICULATE REMOVAL  AND  S02  ABSORPTION  LOOPS.

     THE AIR QUALITY CONTROL  SYSTEM AT  THE  LAWRENCE NO.  a UNIT  CONSISTS  OF TWO-STAGE SCRUBBING FOLL-
OWED BY AN I.D. FAN LEADING  INTO  THE STACK.  THE FIRST SCRUBBING STAGE UTILIZES THE ROD SCRUBBING
APPROACH FOR PARTICULATE REMOVAL.   THE  SECOND STAGE IS A SPRAY  TOWER S02 ABSORPTION LOOP.  OVERFLOW
FROM THE SPRAY TOWER RECIRCULATION  TANK FEEDS INTO THE PARTICULATE LOOP  AND A SIGNIFICANT PORTION OF
THE so2 is THEREFORE REMOVED  IN  THE PARTICULATE  SCRUBBER.

      THE FGD SYSTEMS ON  LAWRENCE  NO. 4  AND  NO. 5 FEATURE FULLY-AUTOMATED CONTROLS.  LIMESTONE FEED
RATE  IS CURRENTLY GOVERNED PRIMARILY BY A PH  MONITORING  SYSTEM,  AND THE  CAPABILITY EXISTS TO TIE IN
THE INLET  AND OUTLET SOS MONITOR  READINGS TO  THE CONTROL SYSTEM.  THERE  ARE ALSO AUTOMATIC DENSITY
METERS  IN  THE LIMESTONE  SLURRY TANKS.

      FOR A SIMPLIFIED  FLOW DIAGRAM  OF  THE LIMESTONE SCRUBBING SYSTEM,  REFER TO APPENDIX 8.  THE
ORIGINAL LIMESTONE  INJECTION  SYSTEM, NOW REPLACED,  IS  ALSO REPRESENTED IN APPENDIX B.

    *A  HISTORY OF PROBLEMS WITH  THE INJECTION SYSTEM AT  LAWRENCE NO. a*

      PROBLEMS WITH  THE  FGD SYSTEM ON BOILER NO.  4  INCLUDED BUILDUP AND PLUGGING OF THE INLET DUCT
WHERE  HOT  GASES  ENTER  THE SCRUBBERS, EROSION  OF  SCRUBBERS WALLS, CORROSION OF SCRUBBERS INTERNALS,
BUILDUP ON  ID FAN ROTORS, AND PLUGGING  OF DRAIN  LINES, MARBLE BEDS, AND  DEMISTERS.  LOW S02 REMOVAL
WAS CAUSED BY OVERBURNING OF  THE LIMESTONE  AND DROPOUT OF THE LIME WITH  THE ASH IN THE BOTTOM OF THE
SCRUBBER.

      THE SCRUBBERS  WERE  MODIFIED IN 1969 BY RAISING THE  DEMISTER AND ADDING SOOT BLOWERS IN THE
 INLET  DUCT  AND REHEATfcR  TO REDUCE PLUGGING.  NEh SPRAY NOZZLES  WERE ALSO INSTALLED.  REHEATER PLUGG-
 ING WAS ELIMINATED  BY  REPLACING  COPPER  REHEAT COILS WITH A CARBON STEEL  UNIT HAVING WIDELY SPACED
FINS.

      MAJOR MODIFICATIONS IN  1970 WERE  SANDBLASTING AND COATING  OF THE INTERIOR OF THE SCRUBBERS, RE-
PLACEMENT  OF  ALL  INTERNAL STEEL  PIPES  WITH  PLASTIC AND FIBERGLASS, AND REPLACEMENT OF STAINLESS
 STEEL DEMISTERS  WITH  FIBERGLASS.  SINCE DEMISTER PLUGGING WAS NOT COMPLETELY ELIMINATED, THE UNIT
WAS   WASHED  MANUALLY  EVERY  NIGHT TO MAINTAIN  THE REQUIRED OUTPUT.

      THE MODIFICATIONS IN THE SUMMER OF 1972  ON  THE TWO  FGD MODULES INCLUDED ENLARGEMENT OF THE CRY-
 STALLIZATION  TANK,  AND INSTALLATION OF  NEW  PLASTIC SPRAY NOZZLES, NEW SLURRY PUMPS AND STRAINERS,
 AND NEW MULTIPLE  MIXERS  IN  THE  TANK.

      PROBLEMS  THAT  REMAINED  INCLUDED CORROSION,  INEFFICIENT DAMPERS, EXPANSION JOINT FAILURE,
 DEMISTER FOULING,  RAPID  EROSION  OF  THE  SLURRY PUMP, AND  VALVE FAILURE.  OPERATION OF THE FGD SYSTEM
 SINCE THE  FALL OF  1973 HAS  BEEN  THE MOST SUCCESSFUL TO DATE.

      OPERATION OF  THE  SCRUBBER  SYSTEM  ON THE  WYOMING COAL HAS PROVED TO  BE MOKE EFFICIENT AND ECON-
OMICAL  THAN  EARLIER OPERATIONS  BECAUSE  A LESSER  DEGREE OF S02 REMOVAL IS REQUIRED FOR COMPLIANCE.
 THE SCRUBBER  SYSTEM IS STILL OPERATING  IN  THE HIGH-SOLIDS MODE  AS AN S02 AND PARTICULATE REMOVAL
 SYSTEM,  NORMAL  MANUAL CLEANING  REQUIREMENTS  HAVE  BEEN REDUCED  TO TWO 4-HOUR SHIFTS PER SCRUBBER
 PER WEEK.

      IN  1974  THIS  UNIT  WAS  AVAILABLE FOR OPERATION 343 DAYS.  FIFTY PERCENT OF THE FUEL CONSUMED WAS
 COAL,  2 PERCENT  FUEL  OIL, AND 48 PERCENT NATURAL GAS.   DURING 1975 THIS  UNIT WAS AVAILABLE FOR OPER-
 ATING 333  DAYS.   SIXTY-FOUR  PERCENT OF  THE  FUEL  CONSUMED WAS COAL, 3 PERCENT FUEL OIL, AND 33
PERCENT NATURAL  GAS.

      BY LATE  1976,  THE  ORIGINAL  EMISSION CONTROL SYSTEM  HAS REPLACED WITH A ROD AND SPRAY TOWER
 SCRUBBER FOR  PARTICULATE AND 302 REMOVAL.   INFORMATION ON THE ORIGINAL AND REPLACEMENT SYSTEM  IS
GIVEN IN THE  FOLLOWING  TABLE.
                                                   61

-------
KANSAS PUwER & LIGHT                                                   LAWRENCE  UNIT  NO.  «

       OPERATING HISTORY - NOW TERMINATED LIMESTONE INJECTION SYSTEM - LAWRENCE  NO. «

                         OPERATING HOURS         AVAILABILITY
MONTH     BOILER      MODULE A   MODULE B      MODULE A   MODULE B

       THE FGD SYSTEM HAS OPERATED SATISFACTORILY FOR OVER A YEAR.  AVAILABILITY  IS REPORTED TO BE
       ADEQUATE FOR THE OPERATION OF THIS STATION.  STATION LOAD IS REDUCED TO 50  PERCENT  EVERY
       NIGHT.  THEREFORE, ONE OF THE MODULES CAN  BE TAKEN OFF-LINE NIGHTLY FOR  CLEANING  OR  REPAIR.
       rtYUMING COAL (0.5 PERCENT SULFUR) IS BEING BURNED IN THE BOILER.  SOME NATURAL GAS  HAS BEEN
       BURNED SINCE JUNE 20.

JUL. 7b                  NOT LOGGED
AUG. 75
       EACH MODULE SHUT DOWN ONCE PER WEEK FOR INSPECTION AND CLEAN-UP.  NO BOILER OUTAGES OCCURRED
       DURING THE JULY-AUGUST PERIOD.

SEP. 75                  N01 LOGGED
OCT. 75

NUV. 75                  NOT LOGGED
DEC. 75

JAN. 76                  NOT LOGGED
FEB. 76
       PRESENT PROJECTIONS 8Y THE UTILITY CALL FOR THIS UNIT TO BE AVAILABLE 330  DAYS DURING 1976.
       THE FUEL CONSUMPTION WILL BE 80 PERCENT COAL, 12 PERCENT NATURAL GAS, AND  fl PERCENT FUEL  OIL.
       THE UTILITY IS REPLACING THIS SCRUBBER SYSTEM WITH A VENTRI-ROD FOLLOWED  BY A  SPRAY TOWER.

MAR. 76
APR. 76

MAY. 76            NO INFORMATION WAS REPORTED BY THE UTILITY FOR THE PERIOD.
JUN. 76

JUL. 76            NO INFORMATION WAS REPORTED BY THE UTILITY FOR THE PERIOD.
AUG. 76

SEP. 76
OCT. 76

NOV. 76            TURBINE OVERHAUL AND REPAIR
DEC. 76
       THE UTILITY REPORTS THAT THE UNIT REMAINED OUT OF SERVICE THROUGHOUT THE REPORT PERIOD  AS A
       SCHEDULED TURBINE OVERHAUL, WHICH COMMENCED IN MID-SEPTEMBER, CONTINUED. THE NEW EMISSION
       CONTROL SYSTEM, CONSISTING OF A ROD SECTION AND SPRAY TOWER SCRUBBING SYSTEM,  HAS BEEN
       INSTALLED ON THIS UNIT.  INITIAL OPERATION OF THE SYSTEM WILL COMMENCE FOLLOWING COMPLETION
       OF THE TURBINE OVERHAUL.  THE UNIT WILL CONTINUE TO FIRE LOW SULFUR WYOMING COAL (0.5X  SULFUR
       10,000 8TU/LB).
                                                  62

-------
KANSAS POWER & LIGHT                                                              LAWRENCE UNIT NO.  4

                OPERATING HISTORY  -  WET  LIMESTONE  SCRUBBING SYSTEM - LAWRENCE NO. 1

JAN. 77        THE NEW LIMESTONE FGO  SYSTEM  BECAME COMMERCIALLY OPERABLE IN EARLY JANUARY 1977.
FEB. 77   THERE HAVE BEEN NO FORCED  OUTAGES  AND NO DOWNTIME SINCE START-UP.  THE UTILITY REPORTS
MAR. 77   THAT BOTH PARTICULATE AND  soa  REMOVALS ARE  QUITE SATISFACTORY.  MINOR PROBLEMS HAVE BEEN
          RELATED TO MAINTAINING DESIRED SOLIDS LEVEL IN THE MAKE-UP TANK.  MODIFICATION PLANS
          INCLUDE CESSATION OF SLURRY DILUTION, WHICH CURRENTLY PRECEDES THE INTRODUCTION OF THE
          FRESH LIMESTONE SLURRY INTO THE  RECIRCULAT ION LOOP.  THE UTILITY PLANS TO PUMP THE 35-
          PERCENT SOLIDS SLURRY DIRECTLY FROM  THE  SLURRY TANK INTO THE REC IRCULATION LOOP.  CURRENT-
          LY SEVERAL DIFFERENT MAKES  OF  SLURRY PUMPS  ARE BEING USED.  ALL ARE FUNCTIONING WELL SO
          FAR.  THE PUMPS HAVE NOT BEEN  IN SERVICE LONG ENOUGH FOR COMPARISONS TO BE DRAWN.

APR.  77        THE SCRUBBER WAS NOT  REQUIRED FOR SERVICE DURING THE REPORT PERIOD BECAUSE NATURAL
MAY   77   GAS WAS FIRED  IN  THE BOILER.   KP&L ANTICIPATES THAT THE NATURAL GAS AVAILABILITY SHOULD
          LAST THROUGHOUT THE  MAJORITY  OF  THE  SUMMER/ REQUIRING NO SCRUBBER PLANT OPERATIONS DURING
          THE PERIOD.

JUN.  77        THE NO. 4 BOILER HAS  BEEN FIRING 100X  NATURAL GAS FOR ALL BUT APPROXIMATELY 8 TO 10
JUL.  77   DAYS SINCE THE BEGINNING OF APRIL  1977.   DURING THE DAYS WHEN COAL WAS FIRED.  1HE  TnO-
          STAGE WET PARTICULATE AND  SG2  REMOVAL SYSTEM HAS BEEN UTILIZED AND OPERATIONS  HAVE BEEN
          SATISFACTORY WITH THE EXCEPTION  OF MINOR PROBLEMS RELATED TO THE MINIMAL USAGE OF  THE
          SYSTEM.  PROBLEMS IN  THE SCRUBBING TRAIN HAVE INCLUDED SOME MIST ELIMINATOR CKACKSf
          PROBLEMS WITH  THE RECYCLE  TANK STRAINER  SCREEN WASH, A COMPRESSOR BREAKDOWN IN THE RECYCLE
          TANK AIR AGITATION  SYSTEM,  AND SOME  SOOT BLOWER PROBLEMS.  IN ADDITION, THE DENVER SLURRY
          PUMPS ARE EXPERIENCING  SOME ON-GOING PROBLEMS, WHILE THE ALLEN-SHERMAN-HOFF PUMPS  ARE
          OPERATING SATISFACTORILY.
               THE UTILITY  IS  PLANNING FOR AN  INTERRUPTION OF GAS SUPPLY IN THE FOURTH QUARTER OF
          THIS YEAR,  AND  THE  RESTART OF  CONTINUOUS COAL-FIRING POWER GENERATION.

 AUG.  77        THE BOILERS  BURNED  NATURAL  GAS  THROUGHOUT AUGUST.  THE MIST ELIMINATOR CRACKS HAVE
 SEP.  77   BEEN REPAIRED,  BUT  THE  RECYCLE TANK  STRAINER PROBLEMS PERSISTED.  THE AIR AGITATION SYSTEM
          COMPRESSOR  WAS  MALFUNCTIONING.  THE  DENVER  SLURRY PUMPS ARE FUNCTIONING ADEQUATELY AT
          PRESENT.  THE  PUMP  GLAND PACKINGS  ARE BEING REDESIGNED.  AS OF 9/15/77 THE UNIT BURNED
 OCT.  77   COAL.   THE  SYSTEM CAPACITY WAS CUT BACK  TO  50 PERCENT 150-55 MW) IN OCTOBER BECAUSE A NEW
 NOV.  77   COOLING  TOWER  IS  BEING  CONSTRUCTED.   ON  NOV. 15 A MAJOR FGD SYSTEM OVERHAUL TOOK PLACE
          WHILE  THE TURBINE WAS DOWN FOR INSPECTION AND THE NEW COOLING TOWER WAS BEING  CONNECTED.
          UNIT  IS  DUE  BACK  ON-LINE IN MID-DECEMBER.
 DEC.  77        THE UNIT  CAME  ON-LINE DECEMBER  208  WITH FULL CAPACITY.  THE CONSTRUCTION  OF THE NEW
          COOLING  TOWER  IS  COMPLETE.  THE  TURBINES WERE BALANCED.

 JAN.  78        THE FGD  SYSTEM  OPERATED WITHOUT ANY PROBLEMS OTHER THAN SOME FREEZING OF  THE  PIPE-
          LINES.   THE  FREEZER  IN  THE DISCHARGE LINE CAUSED CLARIFIER PLUGGING.
                                                   63

-------
                  TABLE 3
PERFORMANCE DESCRIPTION FOR OPERATIONAL FGD SYSTEMS THROUGH  01/78
 UTILITY NAME          KANSAS POWER & LIGHT

 UNIT NAME             LAWRENCE NO 5

 UNIT LOCATION         LAWRENCE KANSAS

 UNIT RATING            tOO MW

 FUEL CHARACTERISTICS  COAL 0.5 PERCENT SULFUR

 FGD VENDOR            COMBUSTION ENGINEERING

 PROCESS               LIMESTONE SCRUBBING

 NEW OR RETROFIT       NEW

 START UP DATE         11/71

 FGD STATUS            OPERATIONAL

 EFFICIENCY,
  PARTICULATES         99 PERCENT


  S0£                  65 PERCENT


 WATER MAKE UP         OPEN LOOP


 SLUUGE DISPOSAL       PLANT SITE DISPOSAL POND


 UNIT COST


 OPERATIONAL           REFER TU THE BACKGROUND INFORMATION SECTION  IN TABLE  3  OF  THIS  REPORT.
  EXPERIENCE           THE ORIGINAL LIMESTONE INJECTION AND TAIL-END SCRUBBING  SYSTEM  IS  STILL
                       IN SERVICE WHILE A NEW ROD-SCRUBBER AND SPRAY TOWER ABSORBER  SYSTEM  IS
                       BEING ERECTED ALONG SIDE THE EXISTING SYSTEM. THE NEW SCRUBBER  PLANT
                       INCLUDES a MODULES EACH CAPABLE OF HANDLING  APPROXIMATELY  sox OF  THE  TO-
                       TAL BOILER FLUE GAS FLOW. THE SYSTEM DESIGNER AND SUPPLIER IS COMBUSTION
                       ENGINEERING. THE UNIT FIRES APPROXIMATELY  UO TONS/HOUR  OF LOW  SULFUR
                       WYOMING COAL HAVING HEAT AND SULFUR CONTENTS OF  10,000  BTU/LB AND  0.5X.
                                               64

-------
                                       BACKGROUND  INFORMATION
                                                 ON
                                            LAWRENCE  NO.  5

     UNIT NO. 5 AT LAWRENCE POWER STATION  IS  A  CYCLIC-LOAD  STEAM BOILER  EQUIPPED  TO  BURN  COAL,
NATURAL GAS SUPPLEMENTED WITH OIL, OR COMBINATIONS OF  THESE FUELS.   THE  BOILER,  PLACED  IN SERVICE  IN
1971, HAS A RATED CAPACITY OF 400 MW WHEN  BURNING  COAL AND  NATURAL  GAS.

     THE COAL NOW BURNED AT THE LAWRENCE POWER  PLANT  IS  A LOW-SULFUR  SOUTHEAST  COAL,  HAVING  AN  AVE-
RAGE HEATING VALUE OF 10,000 BTU/LB  AND SULFUR  AND ASH CONTENTS  OF  0.5 AND  11  PERCENT RESPECTIVELY.

     THE BOILER'S ORIGINAL FGD SYSTEM WAS  SUPPLIED BY  COMBUSTION ENGINEERING  AND  PLACED IN SERVICE
IN 1971.  ORIGINAL EQUIPMENT INCLUDED 8 IDENTICAL  MODULES WITH  A CAPACITY  OF  150,000  SCFM/MODULE.
EACH MODULE CONSISTS OF A SINGLE-STAGE MARBLE BED  SCRUBBER  FOLLOWED BY A CHEVRON-TYPE DEMISTEft  AND
INDIRECT STEAM REHEATER.  ALL THE MODULES  ARE FITTED  WITH BY-PASS DUCTS  AND HYDRAULIC SEAL DAMPERS.
THE PLANT INCLUDES FACILITIES FOR STORING  AND MILLING  LIMESTONE  (COMPOSITION:  93  PERCENT  CALCIUM
CARBONATE, 6 PERCENT SILICA, AND  1 PERCENT MAGNESIUM  CARBONATE).

     SPENT SLURRY FROM THE UNIT ALONG WITH THE  SLURRY  FROM  UNIT  NO. 4 IS SENT  TO  THREE  INTER-
CONNECTED UNLINED SLUDGE DISPOSAL PONDS OF 16,  28, AND 4 ACRES.   COOLING TOWER  SLOWDOWN SUPPLIES
MAKE-UP  WATER TO THE POND SYSTEM.  CLARIFIED  POND  WATER  IS  RECYCLED.  THE SLUDGE  IS NOT  TREATED
FURTHER  AND  IS REPORTED TO SET AND SOLIDIFY IN  THE PONDS.
PROBLEMS AND SOLUTIONS

     PROBLEMS WITH THE FGO SYSTEM ON BOILER NO. 5  WERE SIMILAR  PROBLEMS  TO  THOSE  OF  THE SYSTEM  ON
BOILER  NO. 4:  LOCALIZED CORROSION IN SOME EQUIPMENT,  UNSATISFACTORY  DAMPER OPERATION,  DEMISTER
FOULING, EXPANSION JOINT FAILURE, AND RAPID WEAR OF  SLURRY-RECIRCULATING PUMPS.   IN  ADDITION TO
THESE  PROBLEMS,  BOILER NO. 5  IS PLAGUED WITH  POOR  FLUE GAS  DISTRIBUTION  TO  THE  EIGHT  FGD  MODULES
WHICH,  UNLIKE THE MODULES ON BOILER  NO. 4  ARE ALL  INTERCONNECTED TO A COMMON  STACK.

     FGD SYSTEM  AVAILABILITY  IS ADEQUATE  FOR  THE OPERATION  OF  THIS  STATION.  BECAUSE  THE  STATION
LOAD IS REDUCED  TO FIFTY PERCENT, AS MANY  AS  FOUR  MODULES ARE  SHUT  DOWN  FOR CLEANING  AND  REPAIR EACH
EVENING.

     OPERATION OF THE  SCRUBBER  SYSTEM ON  WYOMING COAL  HAS PROVED TO BE MORE EFFICIENT AND ECONOMICAL
BECAUSE OF  THE LESSER  DEGREE  OF SOa  REMOVAL REQUIRED.

      IN 1974 THE UNIT  WAS  AVAILABLE  FOR OPERATION  338  DAYS*  66  PERCENT  OF  THE  FUEL  CONSUMED WAS
NATURAL GAS,  27  PERCENT  COAL,  AND 6  PERCENT FUEL OIL.   DURING  1975  THE UNIT WAS  AVAILABLE FOR OPER-
ATION  352  DAYS,  FUEL  CONSUMPTION  WAS 45 PERCENT NATURAL GAS,  42  PERCENT  COAL,  AND 13  PERCENT FUEL
OIL.

     KP&L,  IN  ORDER  TO  MAINTAIN SCRUBBING  OPERATIONS FOR THIS  UNIT, IS NOW  FOLLOWING  A  COURSE SIM-
ULAR TO THE  ONE  EMPLOYED FOR  THE  NO. 4  UNIT AT  THIS  STATION.   SPECIFICALLY, A  TWO-TRAIN VENTURI-ROD
SCRUBBER AND SPRAY  TOWER  ABSORBER ASSEMBLY IS BEING  INSTALLED  ALONGSIDE  THE EXISTING  MARBLE-BED
 SYSTEM.  THE MARBLE-BED  UNITS  WILL  REMAIN  IN SERVICE UNTIL  THE  NEW  SPRAY TOWER  SYSTEM HAS BEEN  COMP-
LETED  AND  DUCTED INTO  THE  BOILER  FLUE  GAS  STREAM.   THIS WILL  OCCUR  SOMETIME DURING THE  COURSE OF
 1978.   ADDITIONAL DATA  AND  INFORMATION  IS  PROVIDED IN THE TABLE  THAT  FOLLOWS.   A  FLOW DIAGRAM OF  THE
 INJECTION  SYSTEM IS  PROVIDED  IN  APPENDIX  B.
                                                   65

-------
KANSAS POWER & LIGHT
                                                                       LAWRENCE  UNIT  NO.  5
                OPERATING HOURS
MONTHS        BOILER     FGD MODULES

       WYOMING COAL IS BEING BURNED IN THIS UNIT.  FGD SYSTEM AVAILABILITY  IS REPORTED  T0_f^  *DE"
       QUATE FOR OPERATION OF THIS STATION.  SINCE STATION LOAD IS REDUCED'TO 50  PERCENT  EVERY
       NIGHT, AS MANY AS FOUR MODULES CAN BE SHUT DOWN FOR CLEANING AND REPAIR EACH  EVENING.
       FGD UNITS WERE OFF-LINE MOST OF JUNE FOR MAJOR REBUILDING OF THE SPRAY SYSTEMS  IN  ALL
       MODULES.  SOME OIL WAS BURNED TO ALLOW BYPASSING OF THE REPAIR.

                          NOT LOGGED

       OIL AND GAS WERE BURNED IN JULY AND AUGUST. NO FGD OPERATION.

                          NOT LOGGED

       GAS AND OIL BURNED ON A PART-TIME BASIS DURING SEPTEMBER AND OCTOBER.  BOILER OUTAGE WAS  DUE
       TO INSPECTION, TURBINE REPAIR, AND REPLACEMENT OF THE SLURRY TANK SCREEN.

                          NOT LOGGED
JUL.  75
AUG.  75
SEP. 75
OCT. 75
NOV. 75
DEC. 75
JAN
     76                   NOT LUGGED
       PROJECTIONS BY THE UTILITY FOR THIS UNIT CALL FOR 330 DAYS OF OPERATION IN 1976 WITH FUEL
       CONSUMPTION BEING 60 PERCENT COAL,  25 PESCENT FUEL OIL,  AND 15 PERCENT NATURAL GAS.  LIKE
       UNIT 0, THIS UNIT MAY BE CONVERTED  TO A VENTRI-ROD AND SPRAY TOWER SCRUBBING SYSTEM.
FEB. 76
MAR. 76
                   NO INFORMATION WAS REPORTED BY THE UTILITY FOR THE PERIOD.
APR. 76
MAY. 76
                   NO INFORMATION WAS REPORTED BY THE UTILITY FOR THE PERIOD.
JUN. 76
JUL. 76

AUG. 76
SEP. 76
                   NO INFORMATION WAS REPORTED BY THE UTILITY FOR THE PERIOD.


                   NO INFORMATION WAS REPORTED BY THE UTILITY FOR THE PERIOD.
OCT. 76
NOV. 76

DEC. 76
       THE UTILITY REPORTS THAT THE INSTALLATION OF THE NEW ROD AND SPRAY TOWER SCRUBBING  SYSTEM IS
       NOW IN PROGRESS.  THE SYSTEM WILL INCLUDE TWO SCRUBBING TRAINS, EACH HANDLING 50 PERCENT OF
       THE FLUE GAS CAPACITY.  FOUNDATION AND STRUCTURAL STEEL ERECTION HAS BEEN COMPLETED.   SOME
       OF THE BREECHING HAS BEEN INSTALLED.  THE FGD SYSTEM WILL OPERATE ON A FULLY AUTOMATED BASIS.
       KP&L REPORTS THAT C-E HAS ENCOUNTERED SOME PROBLEMS WORKING OUT AND FINE-TUNING SOME OF THE
       LOGIC CIRCUITS.  THE BOILER FIRES NO.a FUEL OIL IN ADDITION TO LOW SULFUR WYOMING COAL WHILE
       THE NEW SCRUBBING FACILITIES ARE BEING INSTALLED.  THE ORIGINAL INJECTION AND TAIL-END SCRUB-
       BING SYSTEM IS STILL AVAILABLE FOR SERVICE AND OPERATED WHEN THE UNIT FIRES COAL.   THE SYSTEM
       WILL TREAT FLUE GAS RESULTING FROM THE BURNING OF LOW SULFUR CO.5 PERCENT) WYOMING  COAL.
JAN. 77
FEB. 77
MAR. 77
APR. 77
MAY 77
JUN.
JUL.
       KP&L REPORTED THAT CONSTRUCTION OF THE NEW SCRUBBING SYSTEM IS STILL IN PROGRESS.   ALL
       FOUNDATION WORK HAS BEEN COMPLETED.  ERECTION OF THE STRUCTURAL STEEL AND BREECHING  IS  CON-
       TINUING.  THE ORIGINAL SCRUBBING SYSTEM IS STILL AVAILABLE FOR SERVICE.  THE  INJECTION  AND
       TAIL-END SCRUBBER PLANT WAS IN SERVICE AND OPERATED WHEN THE BOILER FIRED COAL.  ERECTION OF
       THE NEW SCRUBBER PLANT IS CONTINUING.  THE MODULES ARE NOW BEING ERECTED AT THE  PLANT SITE,
       PARALLEL TO THE EXISTING MARBLE-BED SYSTEM.
     77
     77
       OPERATION OF THE EXISTING MARBLE BED SCRUBBERS HAS BEEN QUITE SATISFACTORY  AND  NEARLY  PROBLEM
       FREE.  CONSTRUCTION ON THE NEW SCRUBBER PLANT IS CONTINUING.  THE TWO PARALLEL  SCRUBBING
       MODULES, EACH DESIGNED To HANDLE FLUE GAS FROM 200 MW OF GENERATING CAPACITY, ARE  INSTALLED,
       AS ARE THE REHEATER TUBE BUNDLES.  THE CUNNECTINU DUCTWORK IS CURRENTLY GOING IN.   THE EXIST-
       ING MARBLE BED SCRUBBERS WILL BE REMOVED WHEN THE NEW SCRUBBING SYSTEM  IS HEADY  FOR  S02 RE-
       MOVAL OPERATIONS.
AUG.
SEP.
     77
     77
       THE CONSTRUCTION ON THE NEW SCRUBBER PLANT IS CONTINUING ACCORDING TO SCHEDULE  AND  IS  EXPECT-
       ED TO BE COMPLETE BY APRIL 1978.  KP&L INDICATED THAT MOKE DETAILED INFORMATION WILL BE
       AVAILABLE FOR THE NEXT REPORT.
                                                  66

-------
KANSAS POWER & LIGHT
                                                                 LAWRENCE UNIT NO.  5
MONTHS

OCT. 77
NOV. 77
       1
DEC. 77
JAN. 78
        OPERATING HOURS
       BOILER     FGD MODULES
THE SYSTEM OPERATED UNDER NORMAL CONDITIONS THROUGHOUT  OCTOBER  AND  NOVEMBER  WITH NO PROBLEMS.


THE CONSTRUCTION OF TWO NEK VENTURI SCRUBBERS  IS  OVER.   INLET DUCTWORK  IS BEING INSTALLED.
THE OUTLET DUCTWORK WILL BE INSTALLED  ALONG WITH  ADDITIONAL  CONTROLS  DURING  THE SCHEDULED
OUTAGE IN APRIL 78.  PRESENT FGO SYSTEM OPERATED  WITHOUT  ANY PROBLEMS.
                                                    67

-------
                  TABLE 3
PERFORMANCE DESCRIPTION FOR OPERATIONAL FGD SYSTEMS THROUGH   01/78
 UTILITY NAME

 UNIT NAME

 UNIT LOCATION

 UNIT RATING

 FUEL CHARACTERISTICS

 FGO VENDOR

 PROCESS

 NEW OR RETROFIT

 START UP DATE

 FGD STATUS

 EFFICIENCY,
  PARTICULATES
KENTUCKY UTILITIES

GREEN RIVER NUS. 1  2  AND 3

CENTRAL CITY KENTUCKY

  6U MW

COAL  3.8 PERCENT SULFUR

AMERICAN AIR FILTER

LIME SCRUBBING

RETROFIT

 9/75

OPERATIONAL


99.7 PERCENT
  S02
                       80 PERCENT GUARANTEE
 WATER MAKE  UP
                       OPEN LOOP  1.20 GPM/MW
  SLUDGE DISPOSAL
                       PLANT SITE DISPOSAL POND
 UNIT  COST
                      SEE APPENDIX  A, FGD SYSTEM ECONOMICS
  OPERATIONAL
  EXPERIENCE
REFER TO BACKGROUND INFORMATION SECTION IN TABLE 3 OF  THIS  REPORT.
THE SCRUBBER PLANT INSTALLED AT THIS STATION CONSISTS  OF ONE  MODULE
DESIGNED TO REMOVE PARTICULATES (VARIABLE-THROAT VENTURI) AND  S02  (MOBILE
-BED ABSORBER) FROM COAL-FIRED BOILER FLUE GAS. THE SCRUBBER  WAS  DESIGNED
AND SUPPLIED BY AAF. INITIAL SCRUBBER PLANT STARTUP OCCURRED  IN  SEPTEMBER
1975. SCRUBBING OPERATIONS RESUMED IN NOVEMBER FOLLOWING A  5-MONTH  SHUT-
DOWN RESULTING FROM A STRIKE BY PLANT OPERATING PERSONNEL.   THE  SYSTEM
HAS HAD LOW AVAILABILITY BECAUSE OF FROZEN EQUIPMENT.
                                               63

-------
                                       BACKGROUND  INFORMATION
                                                 ON
                                      GREEN  RIVER  POWER  STATION

     THE GREEN RIVER POWER STATION  IS WHOLLY  OWNED AND  OPERATED  BY  THE KENTUCKY  UTILITIES COMPANY
AND SITUATED ON THE GREEN RIVER, NEAR CENTRAL CITY IN MUHLENBERG COUNTY,  KENTUCKY.   THE STATION CON-
SISTS OF FOUR TURBINE GENERATORS AND FIVE  COAL-FIRED BOILERS.  TOTAL  PLANT  POWER-GENERATING CAPACITY
IS APPROXIMATELY 242 MW.

     AS THE RESULT OF A CONTRACT AWARDED BY  KENTUCKY UTILITIES  (KU)  TO AMERICAN  AIR  FILTER (AAF), A
TAIL-END WET LIME SCRUBBING SYSTEM  WAS DESIGNED  AND  INSTALLED ON BOILERS  1,  2,  AND  3 AT THE GREEN
RIVER STATION.

     THE FLUE GAS DESULFURIZATION  CFGD)  AND  PARTICULATE  REMOVAL  SYSTEM CONSISTS  OF  ONE SCRUBBER
MODULE DESIGNED TO HANDLE A MAXIMUM OF 360,000 ACFM  OF  FLUE  GAS  AT  300 F.   THE  BLOW-THROUGH SCRUBBER
MODULE CONTAINS A VARIABLE-THROAT  FLOODED-ELBOW  VENTURI  FOR  FLY  ASH  REMOVAL  AND  A MOBILE BED CON-
TACTOR FOR SULFUR DIOXIDE REMOVAL.  ENTRAINED WATER  DROPLETS ARE REMOVED  VIA A  CENTRIFUGAL DEMISTER
BEFORE DISCHARGE TO A LOCAL STACK.  THE  SLURRY RECYCLE/DISCHARGE SYSTEM CONSISTS OF  ONE COMMON ACID
RESISTANT TANK WITH TWO PARTITIONS  MAKING  A  TOTAL  OF THREE COMPARTMENTS.   COMPLETION OF CHEMICAL
REACTIONS, RECIRCULATION OF SOLUTION AND WASTES  DISCHARGE  ARE CONTROLLED  AND MONITORED HERE.  MECH-
ANICAL COLLECTORS ARE PROVIDED  UPSTREAM  OF THE WET SCRUBBING SYSTEM  FOR PRIMARY  PAftTICULATE MATTER
REMOVAL.

     THE SCRUBBER LINING WAS  INITIALLY "CARBOLINE" WHICH HAD TO  BE  REPLACED  DUE  TO  EXCESSIVE
FLAKING.  IN JANUARY 77, THE  SCRUBBER AND  STACK  WERE RELINED BY  PRECRETE.   THE  L/G  RATIO MAINTAINED
IS 39.5 AND A PH OF 7.8-8 IS  MAINTAINED  AT THE INLET OF  THE  SCRUBBER.   THE  GAS  TEMPERATURE AT  THE
OUTLET IS 115 F WHEREAS THE SLURRY  HAS AN  OUTLET PH  VALUE  OF 5.6-6.   THE  SOLIDS  CONTENT OF THE
RECIRCULATING SLURRY IS 20X.   THE  SCRUBBER INTERNALS ARE POLYURETHANE  PING-PONG  BALLS (1  1/2 IN.
DIA.).  THE RECIRCULATING PUMPS WERE RUBBER  LINED.  THEY WERE REPLACED BY  HIGH  NI ALLOY MATERIAL.

     BOILERS 1, 2, AND  3 ARE  PULVERIZED  COAL-FIRED UNITS SERVICING  TWO TURBINES,  EACH RATED AT 32 MW
(GROSS).  THE FUEL BURNED IN  THESE  UNITS  IS  PRIMARILY A  HIGH SULFUR  WESTERN  KENTUCKY COAL (10,797
BTU/LB., 3.8 TO 4.0 PERCENT SULFUR, 13 TO  14 PERCENT ASH).   THE  FGD  SYSTEM  CAN  BE BYPASSED THROUGH A
SERIES OF DUCTWORK AND  GUILLOTINE  DAMPERS.

     A TURNKEY  CONTRACT FOR THIS PROJECT  WAS AWARDED TO  AAF  IN JUNE  1973.   CONSTRUCTION AND INSTAL-
LATION OF THE SYSTEM WAS COMPLETED  BY MID-SEPTEMBER  1975.  FOLLOWING  GENERAL ELECTRICAL AND MECH-
ANICAL DEBUGGING, WHICH  INCLUDED OPERATION OF THE  AGITATORS  AND  PUMPS, THE  UNIT  WAS  PUT IN SERVICE
ON AIR AND WATER ONLY  IN AUGUST 1975.  DURING THIS OPERATION PERIOD,  THE  FLOW OF  GAS AND LIQUID,
OPERATION OF DAMPERS,  AND SPRAY PATTERNS  WERE MONITORED  AND  CALIBRATED.  NEXT,  THE  SYSTEM WAS
OPERATED ON  AIR AND WATER UNDER NORMAL PROCESS CONDITIONS.   THE  PURPOSE OF  THIS  PHASE OF OPERATION
WAS  TO DETECT ANY EARLY FAILURES OF A MECHANICAL NATURE  PRIOR TO THE  INITIAL FLUE GAS RUN.

     THE FLUE GAS RUN  COMMENCED THE MORNING  OF SEPTEMBER 13, 1975.   INITIAL  OPERATION PROCEEDED ON A
HALF-LOAD BASIS BECAUSE ONE OF  THE  TURBINE GENERATORS WAS  OUT OF SERVICE  FOR OVERHAUL AND REPAIRS.
IN ADDITION, OPERATION  OF THE SCRUBBING  SYSTEM WAS CONDUCTED ON  AN  OPEN-WATER-LOOP  BASIS.  THIS MODE
OF OPERATION  (HALFLOAD, OPEN  LOOP)  CONTINUED INTO  THE FIRST  QUARTER  OF 1976. IN  MARCH, THE SYSTEM
BEGAN OPERATION AT FULL LOAD  CAPACITY IN  A CLOSED-WATER-LOOP MODE.   GUARANTEED  SULFUR DIOXIDE
REMOVAL EFFICIENCY  IS  80 PERCENT FOK 3.8  PERCENT SULFUR  COAL HAVING  A  HEATING VALUE  EQUAL TO OR
GREATER THAN  11,000 BTU/LB.

     ADDITIONAL INFORMATION ON THE OPERATION OF  THIS SYSTEM  IS PRESENTED  IN  THE  PERFORMANCE TABLE
THAT FOLLOWS.   A GENERAL PROCESS FLOW DIAGRAM IS PRESENTED  IN APPENDIX B.
                                                   69

-------
KENTUCKY UTILITIES                                              GREEN RIVER  UNIT  NOS.  1,  2,  AND 3

            TOTAL         BOILER             MODULE           MODULE CALLED     HR.  MODULE
PERIOD  PERIOD (HR)   OPERATION (HR)    AVAILABILITY  (HR)    TO OPERATE  (HR)    OPERATED

DEC. 75      744            398                550                 331              257
AVAILABILITY = 74X
RELIABILITY a 78X
OPERABILITY a 65X
UTILIZATION s 35X
       SYSTEM BECAME OPERATIONAL SEPTEMBER 13, 1975 ON A HALF-LOAD BASIS BECAUSE  OF  TURBINE  OVER-
       HAUL.  THE HALF-LOAD MODE CONTINUED THROUGHOUT THE REPORT PERIOD.  LOGGING OF OPERATING DATA
       BEGAN DECEMBER 1975.

JAN. 76     744             572                312                 456              6"
AVAILABILITY = 42X
RELIABILITY a 14X
OPERABILITY a 11X
UTILIZATION a 9X
       SYSTEM WAS DOWN A TOTAL OF 432 HOURS IN JANUARY.  MAJOR PROBLEMS WERE FAILURE OF THE  RECYCLE
       PUMPS AND FEED TANK AGITATOR.  THAWING AND REPAIR OF NUMEROUS FROZEN LINES,  AND SHUTDOWN  OF
       SUMP PUMPS WAS NECESSARY.

FEB. 76     696             499                486                 499              211
AVAILABILITY = 70X
RELIABILITY = 42X
OPERABILITY * 42X
UTILIZATION * 30X
       THE SYSTEM WAS INOPERATIVE A TOTAL OF 210 HOURS IN FEBRUARY.  OUTAGE WAS DUE  TO REPAIRS OF
       TANK AGITATORS, RECYCLE PUMPS, AND REACTANT PUMPS AND TO CLEANOUT OF REACTANT PUMPS,  SLURRY
       PUMPS, SLAKE TANKS, AND MIX-HOLD TANK.

MAR. 76     744             450                722                 409              386
AVAILABILITY = 97x
RELIABILITY = 95X
OPERABILITY s 85X
UTILIZATION = 52X
       DURING THE REPORT PERIOD ALL THE RUBBER-LINED IMPELLERS WERE REPLACED IN THE PUMPS.

APR. 76     720             522                648                 522             522
AVAILABILITY = 90X
RELIABILITY * 100X
OPERABILITY = 100X
UTILIZATION s 77X
       THE UTILITY MADE A PRIOR COMMITMENT TO RUN AT 100 PERCENT OPERABILITY DURING THE MONTH  OF
       APRIL.

MAY  76     744             456                606                 456             456
AVAILABILITY = SIX
RELIABILITY = 100X
OPERABILITY = 100X
UTILIZATION = 61X

JUN. 76     720            597                 720                 596             589
AVAILABILITY = 100X
RELIABILITY = 99X
OPERA8ILITY a 99X
UTILIZATION = 82X

JUL. 76     744             584                666                 581              574
AVAILABILITY = 90X
RELIABILITY = 99X
OPERABILITY = 98X
UTILIZATION s 72X

AUG. 76     744             744                722                 744             72g
AVAILABILITY = 97X
RELIABILITY = 97X
OPERA6ILITY = 97X
UTILIZATION « 97X
       THE MAJORITY OF THE TOTAL FORCED SCRUBBER OUTAGE TIME OCCURRED BECAUSE OF VIBRATION IN  THF
       SCRUBBER BOOSTER I.D. FAN NECESSITATING SYSTEM SHUTDOWN AND REPAIR
                                                  70

-------
KENTUCKY UTILITIES                                               GREEN RIVEk UNIT NOS. 1, 2, AND 3

            TOTAL          BOILER              MODULE          MODULE CALLED    HR. MODULE
PERIOD  PERIOD (HR)   OPERATION  (HR)     AVAILABILITY (HR)    TO OPERATE (HR)    OPERATED

SEP. 76     720              571                 617                 571             571
AVAILABILITY = 86X
RELIABILITY a IOOX
OPERABILITY a 100X
UTILIZATION = 79X
       HALF-LOAD OPERATIONS  WERE  CONDUCTED THROUGHOUT THE PERIOD BECAUSE OF BEARING PROBLEMS TO ONE
       OF THE TWO TURBINE  GENERATING  UNITS.  MINOR FAN PROBLEMS OCCURRED BUT NO FURCED OUTAGE TIME
       WAS REQUIRED.

OCT. 76     744              699                 744                 699             699
AVAILABILITY - IOOX
RELIABILITY s IOOX
OPERABILITY s IOOX
UTILIZATION a 94X

NOV. 76     720              704                 720                 704             704
AVAILABILITY = IOOX
OPERABILITY = IOOX
RELIABILITY a 98X
UTILIZATION * 98X
        DURING NOVEMBER  AND DECEMBER SOME FLUE GAS WAS BY-PASSED AROUND THE SYSTEM WHILE THE UTILITY
        CONDUCTED A CHECKOUT  OF THE SCRUBBER INTERNALS AND REPLACED SOME OF THE PACKING SPHERES IN
        THE MOBILE BED.

DEC. 76     744              536                 539                 591             517
AVAILABILITY - 73X
OPERABILITY = 97X
RELIABILITY a 87X
UTILIZATION a 70X

JAN. 77     744              744                 698                 744             698
AVAILABILITY a 94X
OPERABILITY a 94X
RELIABILITY f 94X
UTILIZATION a 94X
        NO  PROBLEMS OCCURRED  DURING THE MONTH OF JANUARY.

FEB. 77     672              266                 243                 266             243
 AVAILABILITY a 36X
OPERABILITY = 91X
OPERABILITY a 91X
UTILIZATION a 36X
        DURING THE  MONTH OF FEBRUARY IT WAS FOUND THAT THE CARBOLINE STACK LINER WAS BADLY DETERIOR-
        ATED.  SCRUBBER  AND BOILER OPERATIONS WERE TERMINATED UNTIL THE STACK LINING IS REPAIRED.
        THE BOILER  IS  NOT OPERATED WITHOUT THE SCRUBBER BECAUSE THERE IS NO ESP FOR PARTICULATE
        CONTROL.   A MAY  FIRST RE-START IS CURRENTLY PLANNED.

MAR.  77     744                0                   0                   00
 ALL INDEX  VALUES  a OX

 APR.  77     720              167                 268                  167            164
 AVAILABILITY a 40X
RELIABILITY = 98X
OPERABILITY a 96X
UTILIZATION a 23X
        CURRENT PLANT  LOAD REQUIREMENTS DICTATE THAT OF THE THREE AVAILABLE BOILERS, ONE OR TWO ARE
        ON-LINE AT  A  GIVEN TIME AND THE THIRD IS UNDERGOING MAINTENANCE OPERATIONS.

MAY 77      744             527                 736                  527            513
AVAILABILITY = 99X
RELIABILITY = 98X
OPERABILITY a 96X
UTILIZATION a 69X
        THE STACK WAS  REPAIRED FIRST BY WELDING A BACKUP METAL PLATE TO THE PORTIONS OF THE STACK
        WHERE PITTING  OCCURRED.  THE ENTIRE STACK WAS THEN LINED WITH REFRACTORY COATING CALLED PRE-
        CRETE G-8 BY  AAF.  STACK  REPAIRS WERE COMPLETED MARCH 7.

JUN. 77      720              34                 720                   34             34
AVAILABILITY a IOOX
RELIABILITY a IOOX
OPERABILITY » 100X
UTILIZATION a 5X
        WORK ON THE SCRUBBER  MODULE DURING THE MONTH CONCERNED REPAIRS TO THE UNDERBED DAMPER SYSTEM.
        LEAKING IN THE VENTURI AND LIME SLAKING OPERATIONS WAS ALSO REPAIRED.
                                                   71

-------
KENTUCKY UTILITIES
                                                                GREEN RIVER  UNIT  NOS.  It
                                                                                             AND
PERIOD
JUL. 77
    TOTAL
PERIOD (HR)

     744
                          BOILER
                      OPERATION (HR)
     MODULE
AVAILABILITY (HR)

       744
 MODULE CALLED
TO OPERATE (HR)

        0
                                                                                HR.  MODULE
                                                                                 OPERATED
AVAILABILITY = icox
ALL OTHER INDEX VALUES = OX
       A STRIKE BY PLANT OPERATING PERSONNEL RESULTED  IN NO OPERATIONS  FOR  BOILERS  1,  2«  *ND 3 OR
       THE SCRUBBER MODULE THROUGHOUT THE MONTH.  KU IS CONSIDERING  INCLUDING  A  STACK  GAS REHEAT
       SYSTEM AND MODIFYING THE MIST ELIMINATOR  (HADIAL VANE TO A CHEVRON-TYPE UNIT).
AUG. 77      744             0                 744                   0
AVAILABILITY = 100X
ALL OTHER INDEX VALUES - OX
       THE STRIKE CONTINUED THROUGH THE MONTHS OF AUGUST AND SEPTEMBER.
       HAVE STARTED ON OCTOBER 10.

                             (I                 744                   0
                                                                          THE  PLANT  WAS  KEPORTED TO
SEP. 77      720             0
AVAILABILITY = 10UX
ALL OTHER INDEX VALUES = OX
       UNITS 1, 2, AND 3 AND SCRUBBER REMAINED OUT OF SERVICE BECAUSE OF  THE CONTINUING  PLANT
       STRIKE.

                             0                 744                   0               0
OCT. 77    744               0
AVAILABILITY * icox
ALL OTHER INDEX VALUES = OX
       FGO SYSTEM WAS DOWN THIS MONTH DUE TO A STRIKE, HOWEVER, THE SYSTEM WAS AVAILABLE.
       AND SCRUBBER WERE BACK IN SERVICE IN NOVEMBER.
                                                                                            THE  UNITS
                            332
                                               634
                                                                    332
                                                                                    301
NOV. 77     720
AVAILABILITY = 86X
RELIABILITY = 
-------
                  TABLE 3
PERFORMANCE DESCRIPTION FOR OPERATIONAL  FGD  SYSTEMS  THROUGH  01/78
 UTILITY NAME

 UNIT NAME

 UNIT LOCATION

 UNIT RATING

 FUEL CHARACTERISTICS

 FGD VENDOR

 PROCESS

 NEW OR RETROFIT

 START UP DATE

 FGD STATUS

 EFFICIENCY,
   PARTICULATES
 LOUISVILLE  GAS  &  ELECTRIC

 CANE  RUN  NO 4

 LOUISVILLE  KENTUCKY

  176  MM

 COAL  3.5  -  4.0  PERCENT SULFUR

 AMERICAN  AIR FILTER

 LIME  SCRUBBING

 RETROFIT

  8/76

 OPERATIONAL


 99 PERCENT
   soa
                        65  PERCENT
  MATER  MAKE  UP
 OPEN LOOP
  SLUDGE  DISPOSAL
 PLANT-SITE DISPOSAL POND
  UNIT  COST
SEE APPENDIX A, FGD SYSTEM ECONOMICS
  OPERATIONAL
   EXPERIENCE
 REFER TO THE BACKGROUND INFORMATION SECTION IN TABLE 3 OF  THIS REPORT.
 THE FGD SYSTEM RETROFITTED ON THIS BOILER WAS DESIGNED AND SUPPLIED  BY
 AMERICAN AIR FILTER AND WAS FIRST PLACED IN THE GAS PATH ON AUGUST 7,
 1976.  THE SYSTEM CONSISTS OF TWO PARALLEL MODULES WHICH INCLUDE  MOBILE
 BED CONTACTORS AND OPERATE WITH A CARBIDE LIME ADDITIVE.  FOLLOWING  A
 NUMBER OF MAJOR SYSTEM MODIFICATIONS (CHEVRON-TYPE MIST ELIMINATOR,  OIL
 FIRED REHEAT, PLASITE DUCT LINER, HIGHER L/G), THE SYSTEM  SUCCESSFULLY
 PASSED COMPLIANCE TESTING (85X 502 REMOVAL) ON AUGUST 3 AND 4, 1977.
                                                73

-------
                                       BACKGROUND INFORMATION
                                                 ON
                                           CANE RUN NO. 4

     THE CANE RUN POWER STATION IS OPERATED BY THE LOUISVILLE GAS AND ELECTRIC COMPANY  AND  LOCATED
IN LOUISVILLE, KENTUCKY.  THE PLANT CONSISTS Of SIX ELECTRIC POWER STEAM GENERATING  UNITS  HAVING A
TOTAL STEAM TURBINE NET GENERATING CAPACITY OF 992-MW.

     UNIT NO. 4 IS A COAL-FIRED STEAM GENERATING BOILER WITH A CONTINUOUS NET GENERATING CAPACITY OF
176-MW.  THE UNIT HAS A MAXIMUM POWER GENERATION CAPACITY OF 190-MW.  THE UNIT HEAT  RATE IS JO,030
BTU/KWH.  THE BOILER IS CURRENTLY BURNING COAL WITH A GROSS HEATING VALUE OF  11,500  BTU/LB  AND AVE-
RAGE SULFUR AND ASH CONTENTS OF 3.5-4.0 PERCENT AND 11.0-12.0 PERCENT, RESPECTIVELY.

     THE EMISSION CONTROL SYSTEM FOR THIS UNIT CONSISTS OF AN ELECTROSTATIC PRECIPITATION  (ESP)  UP-
STREAM OF A WET SCRUBBING SYSTEM.  THE ESP PROVIDES PRIMARY PARTICULATE CONTROL WHILE THE WET  SCRUB-
BING SYSTEM PROVIDES ADDITIONAL PARTICULATE REMOVAL AND PRIMARY SULFUR DIOXIDE CONTROL.

     THE FLUE GAS DESULFURIZATION (FGD) SYSTEM CONSISTS OF TWO IDENTICAL PARALLEL SCRUBBING TRAINS
DESIGNED AND SUPPLIED BY THE AMERICAN AIR FILTER CAAF) COMPANY.  THE WET SCRUBBING SYSTEM UTILIZES A
SLURRY OF CARBIDE LIME FOR SULFUR DIOXIDE REMOVAL FROM THE FLUE GAS.  THE CARBIDE LIME  IS A WASTE  8Y
-PRODUCT OBTAINED FROM A NEARBY ACETYLENE MANUFACTURING PLANT.  THE HYDRATED LIME CONTAINS  90.9  TO
92.0 PERCENT CALCIUM HYDROXIDE, 2.0 TO 2.5 PERCENT SILICA, 3.0 TO 8.0 PERCENT CALCIUM CARBONATE,  AND
0.1 PERCENT MAGNESIUM OXIDE.

     EACH SCRUBBING TRAIN IS EQUIPPED WITH A GUILLOTINE-TYPE BY-PASS DAMPER ALLOWING BY-PASSING  OF
THE GAS AROUND THE SCRUBBERS.  EASH 5CRUBBBING TRAIN CONTAINS THE FOLLOWING MAJOR PIECES OF EQUIP-
MENT:  I.D. BOOSTER FAN, UUENCH SECTION,  FLOODED ELBOW, MOBILE BED CONTACTOR, CENTRIFUGAL DEMISTER,
AND A 3-SECTION REACTANT TANK SYSTEM.  THE WASTE DISPOSAL SYSTEM CONSISTS OF A 75-FOOT DIAMETER
THICKENER FOR LIQUID-SOLIDS SEPARATION AND A FLY ASH POND FOR ULTIMATE DISPOSAL OF THE THICKENER
UNDERFLOW.  THE SCRUBBING WASTES ARE STABILIZED WITH FLY ASH AND WATER IS RECYCLED BACK TO  THE PROC-
CESS.  THE ORIGINAL SYSTEM DESIGN DOES NOT INCLUDE STACK GAS REHEAT CAPABILITY.  THE SCRUBBED  GASES
ARE DISCHARGED TO AN EXISTING 250-FOOT, ACID BRICK-LINED STACK.

     THE GAS FLOW RATE IS 370.000 ACFM ol  320 F.  THE OUTLET GAS TEMPERATURE IS 130 F.  A PH  OF 9-9.2
IS MAINTAINED IN THE SCRUBBER WHICH IS LINED WITH PRECRETE AND PLACITE 4005 AND PACKED WITH  1  1/4
IN. DIA. POLYURETHANE BALLS.  THE L/G RATIO VARIES FROM 55 FOW ABOVE 140 MW TO 65 FOR UNDER  100 MW.
THE I.D. FANS ARE SITUATED BEFORE THE SCRUBBER AND CONSUME 1100 HP.

     THE PERFORMANCE TABLE THAT FOLLOWS SUMMARIZES THE OPERATING HISTORY, PROBLEMS/SOLUTIONS AND
MODIFICATIONS SINCE STARTUP.  A SIMPLIFIED PROCESS FLOW DIAGRAM IS PROVIDED IN APPENDIX B OF THIS
REPORT.
                                                  74

-------
LOUISVILLE GAS AND ELECTRIC
                                 F6D SYSTEM PERFORMANCE
                                                                             CANE RUN UNIT NU.
                                                 PERFORMANCE FACTORS (X)
PERIOD   HOURS   BOILER  (HR)   SCRUBBERS  (HR)    OPERABILITY    UTILIZATION
AUG. 76   744       740           666                90             90
       OUTAGE TIME DURING THE  MONTH WAS  DUE  PRIMARILY  TO EQUIPMENT INSPECTIONS,  REPAIR/ REPLACEMENT
       OF AUXILIARY MOTOR PARTS,  AND  DEPLETION OF  ABSORBENT SUPPLY BECAUSE OF A  LATE BAKGE DELIVERY.
       THE SCRUBBING SYSTEM HAS  BEEN  GENERALLY OPERATING AT APPROXIMATELY 50 TO  80 PERCENT FLUE  GAS
       CAPACITY.  SOME MINOR PROBLEMS HAVE  BEEN ENCOUNTERED WITH AUXILIARY EQUIPMENT MOTORS AND
       SPRAY NOZZLES IN  THE MOBILE BED CONTACTOR.   THE SPRAY NOZZLES ARE SPINNEK-VANE COMPONENTS
       ORIGINALLY CONSTRUCTED  OF  PLASTIC.   OPERATING TEMPERATURES AND PRESSURES  HAVE CAUSED THE
       PLASTIC HOUSING TO EXPAND  RESULTING  IN  THE  VANES EXTRUDING OUT THE FRONT  END, SUBSEQUENTLY
       CAUSING A BLOCKAGE OF THE  SLURRY  FEED.   THE NOZZLES  HAVE BEEN REPLACED WITH CERAMIC CON-
       STRUCTED COMPONENTS.
SEP. 7b
          720
                     720
                                  650
                                                    90
                                                                  90
OCT. 76   744        600           540                90            73
       THE SYSTEM WAS  IN  SERVICE  THROUGHOUT  THE  MONTH,  BEING AVAILABLE TO THE BOILER ON A  90 PERCENT
       BASIS.   THE  UNIT WAS  TAKEN OUT  OF  SERVICE ON OCTOBER 25 TO IMPLEMENT ADDITIONAL MODIFICATIONS
       TO THE  SCRUBBING SYSTEM.   MAJOR SYSTEM MODIFICATIONS INCLUDE INCREASING PUMP CAPACITY AND  DE-
       CREASING  PRESSURE  DROP.   THESE  TWO PROBLEMS HAVE HINDERED OPERATION OF THE UNIT AT  FULL LOAD
       CAPACITY.  TO DATE,   THE  MECHANICAL RELIABILITY  OF THE SYSTEM,  AS A FUNCTION OF SERVICE TIME
       VERSUS  OUTAGE TIME,  HAS  BEEN  VERY  GOOD.
 NOV.  76    720
                                                    95
 DEC.  76    744                                       90
       THE SYSTEM  INCURRED  NO MAJOR  PROBLEMS OR UPSETS DURING THE REPORT  PERIOD.
       SLURRY  IS EMPLOYED  AS  THE  SULFUR DIOXIDE ABSORBENT.
                                                                           CARBIDE LIME
 JAN.  77    744        00                 00
        DURING  JAN.l  - JAN.11,  THE SCRUBBER WAS UTILIZED 95 PERCENT OF THE TIME.  THEN THE OHIO RIVER
        BECAME  IMPASSABLE DUE TO ICE FORMATION AND THIS CAUSED THE CESSATION OF BARGE DELIVERIES OF
        LIME.

 FEB.  77    672        00                 00
        DURING  FEBRUARY,  THE SCRUBBER WAS ONLY OPERATED FOR TWO 4-HOUR PERIODS TO PREVENT TOTAL
        FREEZE-UP.
 MAR.  77
           744
             432
            (AFTER
           RESTART)
 358
 (AFTER
RESTART)
  «3X
 (AFTER
RESTART)
 63%
 (AFTER
RESTART)
        IN MARCH,  THE SCRUBBER CAME BACK ON-LINE AT 10 AM,  ON MARCH 14TH,  AND HAS RUN CONTINUOUSLY
        THROUGH THE END OF THE PERIOD.  FROM THE 14TH THROUGH THE END OF THE MONTH,  THERE WAS ONE
        PERIOD OF  SCRUBBER BY-PASS, WHEN DC SUPPLY TO THE BY-PASS HAD TO BE REPAIRED.
 APR.  77
 MAY  77
        THE SCRUBBER SYSTEM RAN FOR THE FIRST 18 DAYS IN APRIL,  WITH A RELIABILITY OF 95X.   FROM THAT
        TIME (APRIL 18)  THROUGH AN EXPECTED DATE OF JULY Id, THE SCRUBBER SYSTEM WILL BE DOWN FOR THE
        FOLLOWING MODIFICATIONS:
        1.   TO REMOVE DEMISTER AND REPLACE WITH A CHEVRON TYPE.
        2.   TO INCREASE  L/G BY ADDING A NEW SPRAY HEADER.
        3.   TO ADD DIRECT,  OIL-FIRED REHEAT, AND
        4.   TO REPLACE THE  LINING IN THE SYSTEM FROM THE DEMISTER THROUGH THE STACK WITH PLASTITE
            4005 TO BE INSTALLED BY GENERAL COATINGS (THE ORIGINAL LINING WAS BUBBLING, BUT HAD NOT
            YET FAILED;  FAILURE SEEMED IMMINENT WITHIN 4-5 MONTHS).
        SYSTEM REMAINED  OUT OF SERVICE PENDING COMPLETION OF SYSTEM MODIFICATIONS.
 JUN. 77

 JUL. 77
    744      360         324           90           90
            (AFTER      (AFTER        (AFTER       (AFTER
           RESTART)    RESTART)     RESTART)     RESTART)
SYSTEM MODIFICATIONS WERE COMPLETED AND THE SCRUBBER PLANT WAS PLACED BACK IN SERVICE ON JULY
17.  ON AUGUST 4 THE SYSTEM UNDERWENT AND SUCCESSFULLY COMPLETED TESTING FOR COMPLIANCE WITH
LOCAL (JEFFERSON COUNTY) AND FEDERAL  S02 AIR EMISSION REGULATIONS.  THE ABOVE-MENTIONED MOD-
IFICATIONS ENABLED THE SYSTEM TO EXCEED THE 85X S02 REQUIREMENT (JEFFERSON COUNTY) AND FED-
ERAL STANDARD (1.2 LB/MM BTU).  ACTUAL TEST RESULTS INDICATED AN 86 TO 89X S02 REMOVAL EF-
FICIENCY FOR 3.3 TO 3.4X SULFUR COAL, WHICH IS EQUIVALENT TO AN OUTLET EMISSION VALUE OF
0.8 LB/MM BTU HEAD INPUT.  ALL TESTING WAS PERFORMED BY EPA PERSONNEL.
 AUG.  77
            744
                     657
                                 588
                                               94
                                                            93
 SEP.  77     720       529         524           99           99
        THE  FGD  SYSTEM WAS FURTHER TESTED USING METHOD 6 BY FEDERAL EPA AND WAS OFFICIALLY APPROVED
        TO HAVE  ACHIEVED COMPLIANCE.  THE SYSTEM PERFORMED VERY WELL DURING THIS PERIOD.
                                                   75

-------
LOUISVILLE GAS AND ELECTRIC                                     CANE RUN  UNIT  MO.  4

                                                PERFORMANCE FACTORS  cx>
PERIOD   HOURS   BOILER (MR)  SCRUBBERS (HR)   OPERABILITY   UTILIZATION

OCT. 77    744      677         662           9ft           69
       EPA MAY CONTINUE TO TEST THROUGHOUT JANUARY.  NO REAL PROBLEMS ENCOUNTERED  IN  MAINTAINING
       COMPLIANCE.

NOV. 77   720       483         454           94           63

DEC. 77   744       715         608           85           82

JAN. 78                                       67           67
       NO PROBLEMS OCCURRED DURING THIS PERIOD TO CREATE ANY FGD DOWNTIME.  DURING DECEMBERf
       "AIKCO", THE LIME SUPPLIER, HAD 1200 FT OF THEIR FEED LINE FREEZE  UP.   LIME BECAME  UNAVAIL-
       ABLE FOR A TIME BUT THERE WERE NO SCRUBBER BREAKDOWNS,
                                                  76

-------
                  TABLE 3
PERFORMANCE DESCRIPTION FOR OPERATIONAL F60  SYSTEMS  THROUGH   01/78
 UTILITY NAME

 UNIT NAME

 UNIT LOCATION

 UNIT RATING

 FUEL CHARACTERISTICS

 FGD VENDOR

 PROCESS

 NEW OR RETROFIT

 START UP  DATE

 FGO STATUS

 EFFICIENCY,
   PARTICULATES
LOUISVILLE  GAS  &  ELECTRIC

PADDYS  RUN  NO fc

LOUISVILLE  KENTUCKY

   65  MW

COAL  3.5  -  «.0  PERCENT  SULFUR

COMBUSTION  ENGINEERING

LIME  SCRUBBING

RETROFIT

  a/73

OPERATIONAL


99 PERCENT
   soe
                        60  PERCENT
  WATER  MAKE  UP
 OPEN LOOP 0.7 GPM/MW
  SLUDGE  DISPOSAL
                        HAULAWAY  TO BORROW PIT
  UNIT COST
  OPERATIONAL
   EXPERIENCE
SEE APPENDIX A, FGD SYSTEM ECONOMICS
 REFER TO THE BACKGROUND INFORMATION SECTION IN TABLE 3 OF  THIS  REPORT,
 THIS SCRUBBING SYSTEM WAS DESIGNED BY COMBUSTION ENGINEERING  AND  PLACED
 IN SERVICE IN APRIL 1973.  THE FGD SYSTEM CONSISTS OF TWO  2-STAGE MARBLE
 BED ABSORBERS WHICH ARE DESIGNED TO USE CARBIDE LIME ADDITIVE AS  THE
 SCRUBBING REAGENT.  PADDYS RUN NO.  is A PEAK-LOAD UNIT THAT  OPERATES
 ONLY DURING DEMAND PERIODS.  AN EXTENSIVE EPA SCRUBBER/SLUDGE EVALUATION
 STUDY WAS COMPLETED IN AUGUST 1977.
                                                77

-------
                                       BACKGROUND INFORMATION
                                                 ON
                                         PADDY'S RUN NO. 6

     PADDY'S RUN POWER STATION IS LOCATED IN LOUISVILLE, KENTUCKY.  THE PLANT HAS  SIX  ELECTRIC  POWER
GENERATING UNITS WITH A TOTAL RATED CAPACITY OF 320 MW. UNIT NO. 6 IS RETROFITTED  WITH  A  CARBIDE
LIME-BASED FSD SYSTEM.

     UNIT NO. 6 IS A PEAK LOAD COAL-FIRED BOILER. MANUFACTURED BY FOSTER WHEELER AND INSTALLED  IN
1950.  THIS UNIT FIRES COAL WITH A GROSS HEATING VALUE OF 11,500 BTU/LB AND AVERAGE SULFUR  AND  ASH
CONTENTS OF 3.7 PERCENT AND 13 PERCENT, RESPECTIVELY.

     THE FGD SYSTEM CONSISTS OF TWO MODULES.  EACH HANDLES 175,000 ACFM OF 350 F FLUE GAS.   EACH
MODULE IS MADE UP OF TWO STAGES OF 3-INCH MARBLE BEDS, FOLLOWED BY A TWO-STAGE CHEVRON-TYPE  DEMISTER
THE GAS IS REHEATED BY DIRECT COMBUSTION OF  NATURAL GAS.  AN EXISTING ELECTROSTATIC PRECIPATATOR
CESP, RESEARCH-COTTRELL) IS INSTALLED UPSTREAM OF THE SCRUBBING SYSTEM PROVIDING PRIMARY  CONTROL OF
PARTICULATE EMISSIONS.  THIS UNIT OPERATES WITH A 99.1 PERCENT PARTICULATE REMOVAL EFFICIENCY.
PARTICULATE LOADING AT THE ESP OUTLET IS 0.05 GR/SCF.

     THE SYSTEM UTILIZES A SLURRY OF CARBIDE LIME AS THE SULFUR DIOXIDE ABSORBENT.  THE CARBIDE
LIME, A WASTE BY-PRODUCT OBTAINED FROM A NEARBY ACETYLENE MANUFACTURING PLANT CONTAINS  90 TO 92
PERCENT CALCIUM HYDROXIDE, 2.0 TO 2.5 PERCENT SILICA, 3.0 TO 8.0 PERCENT CALCIUM CARBONATE,  AND  0.1
PERCENT MAGNESIUM OXIDE.

     THE UNIT OPERATES IN A CLOSED-LOOP MODE.  THE SULFUR DIOXIDE IS ABSORBED IN THE MARBLE  BED  BY A
SLURRY OF CALCIUM SULFITE TO FORM A MIXTURE  OF CALCIUM SULFITE/BISULFITE.  EFFLUENT FROM  THE MARBLE-
BED TOWER IS CONVERTED IN THE REACTION TANK  TO CALCIUM SULFITE BY THE ADDITION OF CALCIUM HYDROXIDE.
HALF OF THE REACTION TANK EFFLUENT IS RETURNED TO THE ABSORBER TOWERS WHILE THE OTHER HALF  IS FED TO
A CLARIFIER TANK.  THE CALCIUM SULFITE CRYSTALS PRECIPITATE  WITH THE AID OF A FLOCCULANT, WHICH  is
ADDED AT THE RATE OF 4 TO 7 PPM.  THE OVERFLOW IS RETURNED TO THE REACTION TANK.  THE UNDERFLOW,
CONTAINING 22 TO 21 PERCENT SOLIDS, IS STABILIZED BY MIXING  IT WITH LIME.  APPROXIMATELY 60  TO 100
POUNDS OF LIME ARE USED PER TON OF DRY SOLIDS OF SLUDGE.  THE FIXED SLUDGE IS TRANSPORTED BY TRUCKS
TO A 10-ACRE OFF-SITE LANDFILL AREA.

     ON-SITE CONSTRUCTION OF THE FGO SYSTEM  COMMENCED IN JUNE 1972 AND WAS COMPLETED BY APRIL 1973.
INITIAL STARTUP OCCURRED ON APRIL 5, 1973.  SYSTEM SHAKEDOWN WAS COMPLETED BY JULY 1973.  A SUMMARY
OF THE SYSTEM'S PERFORMANCE HISTORY IS PROVIDED IN THE TABLE THAT FOLLOWS.  A SIMPLIFIED PROCESS
FLOW DIAGRAM IS PROVIDED IN APPENDIX B OF THIS REPORT.
                                                 78

-------
LOUISVILLE GAS & tLECTRIC
                                     FGD SYSTEM OPERABILITY
                                                                  PADDY'S RUN UNIT NO. fa
          OPERABILITY  (X)
MONTH    MODULE A  MODULE  B
APR. 73    18        56
MAY  73     11
JUN. 73      1
 JUL. 73
 AUG.  73     53
 SEP.  73

 OCT.  73
 NOV.  73
 DEC.  73
 AUG.  74
 SEP.  75
 OCT.  75
 MAR.  76
 APR.  76
                      65
 85

 49
 35
 44
 JAN.  74      0
 THROUGH
 JUL.  74      0
            50
 SEP.  74     0

 OCT.  74   100
 NOV.  74
 THROUGH
 AUG.  75
 12

 94
100
 78
            0

            0

           77


            0

          100
100
100
 NOV. 75   100
 DEC. 75    90
100
100
          100
           90
 JAN. 76   100       100
 FEB. 76      NO DEMAND
   NO DEMAND
   NO DEMAND
MODULES WERE OPEHATED ONE AT A TIME, WITH FREQUENT  SHUTDOWNS FOR  IN-
SPECTION OF EQUIPMENT AND MINOR REPAIRS.

SINGLE-MODULE OPERATION CONTINUED THROUGH MAY  19, WHEN  THE  UNIT WAS
SHUT DOWN FOR MODIFICATIONS.  THt MOST  SIGNIFICANT  MUDIFICATION WAS
INSTALLATION OF EQUIPMENT FOR INJECTION OF  A FLOCCULATING AGENT INTO
THE CLARIFIER TANK.

OPERATION WAS INTERMITTENT FHOM JUNE 19 TO  JULY  11  BECAUSE  OF MECHAN-
ICAL PRObLEMS WITH THE SLURRY HUMPS.

DURING A SCHEDULED OUTAGE FRUM JULY  12  THHUUGH AUGUST 1, SEVERAL
REPAIRS WERE MADE TO THE LIME SLURRY MAKE-UP SYSTEM.  A DISINTEGRATOR
UNIT WAS INSTALLED TU REDUCE PLUGGING OF STRAINERS  AND  SLURRY CONTROL
VALVES.

THE OPERATION WAS CONTINUOUS FROM AUGUST 2  TO  AUGUST  IB EXCEPT FOR A
BRIEF SHUTDOWN DUE TO A BOILER-RELATED  PROBLEM.  FRUM AUGUST 19 TO
SEPTEMBER 5, THE SYSTEM WAS SHUT DOWN TO REPLACE THE  CLARIFIER'S
UNDERFLOW LINE WITH ONt UF LARGER DIAMETER  AND TO INSTALL ADDITIONAL
PUMP CAPACITY IN THE CLARIFIER'S OVERFLOW SYSTEM.

THE UNIT OPERATED CONTINUOUSLY BETWEEN  SEPTEMBER 6  AND  SEPTEMBER  20
EXCEPT FOR  A 7-HOUR SHUTDOWN TO REPAIR  A MARBLE  BED SUPPORT PLATE.
THE UNIT WAS SHUT UOWN THE REMAINDER OF THE MONTH.  THE FGO SYSTEM
REMAINED IN SERVICE  TO DEC. 20 AFTER WHICH THE  BOILER  AND  THE SCRUB-
BER MODULES WERE SHUT DOWN BECAUSE OF NO DEMAND  (THIS IS A  PEAKING-
LOAD BOILER) .

BOILER SHUT DOWN BECAUSE OF NO DEMAND.
           UNIT HAS BEEN UN AND OFF FREQUENTLY DUE TO FLUCTUATION IN POWER DE-
           MAND.

           BOILER DOWN BECAUSE OF NO DEMAND.

           BOILER TURNED ON SPECIFICALLY TO PERFORM LIMESTONE TESTS ON FGD
           SYSTEM.

           NO DEMAND
BOILER AND FGD SYSTEM OPERATIONAL ALL OF SEPTEMBER AND FIRST TWO
WEEKS  IN OCTOBER.  SYSTEM OUTAGE DURING THE LAST  TWU WEEKS OF OCTOBER
WAS DUE PRIMARILY  TO BREECHING  IN THE BOILER SECTION.  OPERABILITY
FOR BOTH MODULES DURING  THE OPERATIONAL PERIOD WAS 100 PERCENT
(BASED UPON LG&E'S PEAK  LOAD DETERMINATION).  302 REMOVAL WAS RE-
PORTED TO BE OVER  98 PERCENT.

BOILER AND SCRUBBER SYSTEM RAN  MOST OF  THE REPORT PERIOD ON A MONDAY-
THROUGH-FRIDAY BASIS.  TWO MINOR OUTAGES IN DECEMBER WERE DUE TO
MALFUNCTION AND REPAIR OF THE DUAL STRAINER SWITCH SHAFT IN THE BOT-
TOM OF THE SCRUBBER MODULE.

S02 REMOVAL EFFICIENCY WAS REPORTED TO  BE 99 PERCENT DURING JANUARY.
THE SYSTEM WAS SHUT DOWN  IN EARLY FEBRUARY IN PREPARATION FOR AN EPA
SCRUBBER/SLUDGE STUDY SCHEDULED FOR JUNE OR JULY.  THE SCRUBBER WILL
NOT BE OPERATED UNTIL THE START OF THE  STUDY PROGRAM UNLESS THE
BOILER IS REQUIRED FOR PEAKING  POWER DEMANDS.  HIGHLIGHTS OF THE
SCRUBBER/SLUDGE STUDY PROGRAM ARE AS FOLLOWS:
     6 MONTHS DURATION.
     ONE SCHEDULED SHUTDOWN FOR TEST MODIFICATIONS.
     DELIBERATE HIGH CHLORIDE CONCENTRATION OPERATION.
     MGO INNOCULATION.
     EXTENSIVE SLUDGE STUDY:  FIXATION, LEACHATES, SEASONAL VARIA-
     TIONS.

THE UNIT DID NOT OPRATE  DURING  THE REPORT PERIOD  IN ANTICIPATION OF
THE EPA SCRUBBER/SLUDGE  STUDY.  THE UTILITY IS NOW COMPLETING SYSTEM
MODIFICATIONS FOR  THE OPERATION OF THE  TEST PROGRAM.
                                                    79

-------
LOUISVILLE GAS AND ELECTRIC
                                    FGD SYSTEM OPERABILITY
                                                           PADDY'S RUN UNIT NO. 6
          OPERABILITY U)


MONTH    MODULE A  MODULE B


MAY  76   100       100
JUN. 76
JUL. 76   100
AUG. 76   100
SEP. 76
OCT. 76
NOV. 76
DEC. 76
 JAN.
 FEB.

 MAR.
 APR.
 MAY
77
77
77
77
77
 JUN. 77
 JUL. 77
 AUG. 77
               100
               100
             NO DEMAND
      99
      99
99
99
SEP. 77 NOT OPERATIONAL


OCT. 77 NOT OPERATIONAL


NOV. 77 NOT OPERATIONAL
THIS PEAK LOAD UNIT WAS OPERATED PART OF THE TIME DURING THE REPORT
PERIOD (APPROXIMATELY 2 WEEKS IN MAY AND 2 WEEKS IN JUNE).  THE
SCRUBBER WAS AVAILABLE TO THE BOILER 100 PERCENT OF THE TIME.  S02
REMOVAL EFFICIENCY WAS 96 TO 99 1 DURING THIS OPERATING SEGMENT.

THE UNIT WAS OPERATIONAL PART OF THE TIME DURING THE JULY-AUGUST
PEUIOD.  THE SCRUBBING SYSTEM WAS AVAILABLE TO THE BOILER ON A 100
PERCENT BASIS.  NO MAJOR SCRUBBER-RELATED PROBLEMS WERE ENCOUNTERED.

THE UNIT DID NOT OPERATE THROUGHOUT SEPTEMBER AND THE FIRST 3 WEEKS
OF OCTOBER.  THE EPA-FUNDED SCRUBBER/SLUDGE STUDY PROGRAM COMMENCED
OCTOBER 25.  THE INITIAL PHASE OF THE PROGRAM CALLS FOR OPERATIONS
TO PROCEED FOR A 20 TO 30-DAY PERIOD WITH CARBIDE LIME SCRUBBING
ABSORBENT.  FOLLOWING COMPLETION OF THIS RUN, THE UNIT WILL BE SHUT
DOWN AND MODIFICATIONS WILL BE INCORPORATED INTO THE SYSTEM FOR
OPERATION WITH COMMERCIAL GRADE (HIGH CALCIUM) LIME.

THE UNIT WAS IN SERVICE DURING THE REPORT PERIOD.  THE SCRUBBING
SYSTEM OPERATED 99.5 PERCENT OF THE TIME THE BOILER WAS IN SERVICE.
CARBIDE LIME WAS EMPLOYED AS THE SOa ABSORBENT. THE HIGH CALCIUM
(VIRGIN) LIME RUN, SCHEDULED AS PART OF THE SCRUBBER/SLUDGE STUDY,
WILL COMMENCE ON MARCH 1, 1977.

BECAUSE OF SEVERE WEATHER CONDITIONS, THERE WERE NO BOILER OPERA-
TIONS AND NO SCRUBBER OPERATIONS UNTIL MARCH 15, 1977.
IN MID MARCH, LG&E  BEGAN TESTS FOR EPA WITH REGULAR LIME,  ONE OF
THE OBJECTIVES OF  THE TEST WAS TO DETERMINE WHETHER THERE WERE
APPRECIABLE DIFFERENCES BETWEEN REGULAR LIME AND CARBIDE LIME AT
THIS FACILITY.  DURING OPERATION WITH REGULAR LIME, SCALING PROB-
LEMS OCCURRED WHICH INDICATES THAT THE SCALING RESULTED FROM
INCREASED OXIDATION LEVELS.  AVAILABLE OPTIONS FOR CONTROLLING
SCALING WERE LIMITED BY THE FIXED DESIGN FEATURES OF THE SCRUBBER
HARDWARE.  THE OPTION SELECTED WAS ADDITION OF MGO TO THE SCRUBBING
MEDIUM.  WHEN MGO WAS ADDED, THE SCALING PROBLEM WAS ELIMINATED,
ALLOWING COMPLETION OF THE TEST PROGRAM.

THE SCRUBBER/SLUDGE EVALUATION STUDY CONTINUED DURING THE PERIOD.
THE SCRUBBER PLANT (ONE MODULE IS BEING UTILIZED FOR THIS EXPERI-
MENTAL PROGRAM) WAS IN SERVICE ON A VIRTUALLY CONTINUOUS BASIS FROM
JUNE 18 TO AUGUST 8, OPERATING ON MAGNESIUM INNOCULATED COMMERCIAL
LIME.  SYSTEM OPERABILITY DURING THIS PERIOD WAS APPROXIMATELY 9&x.
S02 REMOVAL EFFICIENCY WAS MEASURED IN EXCESS OF 99.5X.  THE SYSTEM
WAS SHUTDOWN AT THIS POINT TO PERFORM A NUMBER SCHEDULED MODIFICA-
TIONS TO THE SYSTEM FOR TEST PURPOSES.  SPECIFICALLY,  MODIFICATIONS
ARE BEING IMPLEMENTED TO THE SYSTEM IN ORDER TO BYPASS THE REACTION
TANK IN ORDER TO CONDUCT A SHORT TERM RETENTION TIME TEST.   THE TEST-
ING WAS COMPLETED IN AUGUST 77 AFTER THE MODIFICATIONS WERE MADE.

THE UNIT IS CURRENTLY NOT OPERATING DUE TO LACK OF POWER REQUIREMENT.

THE UNIT IS CURRENTLY NOT OPERATING DUE TO LACK OF POWER REQUIREMENT.

THE UNIT IS CURRENTLY NOT OPERATING DUE TO LACK OF POWER REQUIREMENT.
DEC. 77 NOT OPERATIONAL
       THE UNIT IS CURRENTLY NOT OPERATING DUE TO  LACK OF POWER REQUIREMENT.


JAN. 78 NOT OPERATIONAL
       THE UNITS IS CURRENTLY NOT OPERATING DUE TO LACK OF POWER REQUIREMENT.
                                                  80

-------
                  TABLE 3
PERFORMANCE DESCRIPTION FOR OPERATIONAL  FGD  SYSTEMS  THROUGH   01/78
 UTILITY NAME

 UNIT NAME

 UNIT LOCATION

 UNIT RATING

 FUEL CHARACTERISTICS

 FGD VENDOR

 PROCESS

 NEW OR RETROFIT

 START UP  DATE

 FGD STATUS

 EFFICIENCY,
   PARTICULATES
MINNKOTA POWER COOPERATIVE

MILTON R. YOUNG NO. 2

CENTER NORTH DAKOTA

 450 MM

LIGNITE 0.7 PERCENT SULFUR

ADL/COM6USTION EQUIP ASSOCIATE

LIME/ALKALINE FLYASH SCRUBBING

NEW

 9/77

OPERATIONAL


99,6 PERCENT
   SO?


  MATER  MAKE  UP
                        75  PERCENT
CLOSED LOOP
  SLUDGE  DISPOSAL
                        PLANT  SITE/MINE FILL
  UNIT  COST
  OPERATIONAL
   EXPERIENCE
                       SEE APPENDIX A,  F6D SYSTEM ECONOMICS
REFER  TO  THE BACKGROUND  INFORMATION SECTION  IN TABLE 1 OF THIS REPORT.
THIS LIME/ALKALINE FLYASH SCRUBBING SYSTEM WAS DESIGNED AND SUPPLIED BY
ADL/CONTRUCTION EQUIPMENT ASSOCIATEES. IT CONSISTS OF A COLD-SIDE ESP
FOLLOWER  BY TWO SPRAY  TOWERS.  MIST ELIMINATION  IS PROVIDED BY A WASH
TRAY ANO  CHEVRON  ARRANGEMENT.  25X FLUE GAS  BYPASS PROVIDES STACK GAS RE-
HEAT.   THE UNIT FIRES  A  LOW-SULFUR NORTH DAKOTA  LIGNITE WITH AN AVERAGE
ASH CONTENT OF 8  PERCENT, SULFUR CONTENT OF  0.7  PERCENT, AND HEAT CONTENT
OF 6500 BTU/LB.
                                                81

-------
                                     BACKROUND INFORMATION ON
                                       MILTON R. YOUNG NO. 2

     THE MILTON R. YOUNG POWER STATION, OWNED AND OPERATED BY MINNKOTA POWER COOPERATIVE  AND
BUTTE ELECTRIC COOPERATIVE, IS LOCATED NEAR CENTER, NORTH DAKOTA, APPROXIMATELY  30  MILES
OF BISMARCK.  THIS MINE-MOUTH PLANT, WHICH HAS A TOTAL OPERATING POWER-GENERATING CAPACITY  Of  690
MW, CONSISTS OF TWO SEPARATE COAL-FIRED, STEAM-TURBINE, GENERATING UNITS.  UNIT  1 IS  RATED  235 MW.
UNIT 2 IS RATED 440 MW.  THE BOILERS ON BOTH UNITS FIRE NORTH DAKOTA LIGNITE FROM
NEARBY MINES.  AVERAGE CHARACTERISTICS OF THIS COAL ARE 6500 BTU/L8, 0.7 PERCENT SULFUR,  AND 7.5
PERCENT ASH.  BOTH UNITS ARE FITTED WITH ELECTROSTATIC PRECIPITATORS (ESP'S) FOR PARTICULATE CON-
TROL.  UNIT 2 IS ALSO EQUIPPED WITH A FLUE GAS DESULFURIZATION (FGD) SYSTEM FOR  SULFUR  DIOXIDE (802)
CONTROL.

     BOILER 2 IS A CYCLONE-FIRED, STEAM-GENERATING UNIT SUPPLIED BY 8ABCOCK AND  WILCOX.   THE ESP, A
COLD-SIDE UNIT SUPPLIED BY WHEELABRATOR-FRYE, PROVIDES PRIMARY PARTICULATE CONTROL.   TWO  SPRAY
TOWERS, WHICH UTILIZE FLY ASH ALKALI AND LIME SUPPLEMENT AS SCRUBBING REAGENTS,  PROVIDE PRIMARY 802
CONTROL.  THIS FGD PROCESS HAS DESIGNED ANO SUPPLIED BY COMBUSTION EQUIPMENT ASSOCIATES AND ARTHUR
D. LITTLE (CEA/ADL).  DESIGN CRITERIA ANO OPERATING PARAMETERS FOR THIS FULL-SCALE  FGD  SYSTEM  WERE
DETERMINED DURING AN EXTENSIVE PILOT PLANT (5000 ACFM) TEST PROGRAM CONDUCTED BY THE  OWNING/OPER-
ATING UTILITY COMPANIES AND THE SYSTEM SUPPLIER IN CONJUNCTION WITH THE MINNESOTA POWER ANO LIGHT
CO. AND GRAND FORKS ENERGY RESEARCH CENTER.  THE EMISSION CONTROL SYSTEMS, COMPLETE WITH  DISPOSAL
SYSTEMS FOR WASTE SOLIDS AND WASTEWATER, ARE DESCRIBED BRIEFLY IN THE FOLLOWING  PARAGRAPHS.

     BOILER FLUE GAS (1.8 MILLION ACFM AT 340 F) FIRST PASSES THROUGH THE ESP, WHERE  PRIMARY PAKTIC-
ULATE REMOVAL TAKES PLACE.  PARTICULATE LOADING IN THE FLUE GAS AT THE INLET TO  THE ESP RANGES FROM
0.70 TO 1.50 GR/SCF ANO AVERAGES APPROXIMATELY 1.15 GR/SCF.  THE ESP IS DESIGNED TO REMOVE 99.5 PER-
CENT OF THE INLET PARTICULATE MATTER, WHICH MEANS THE OUTLET LOADING WILL AVERAGE 0.005 GR/SCF.
AFTER IT PASSES THROUGH THE ESP, 85 PERCENT OF THE FLUE GAS IS ROUTED TO THE FGO SYSTEM.  BASED ON A
MAXIMUM SULFUR CONTENT OF 1.3 PERCENT IN THE COAL, APPROXIMATELY 1900 PPM (DRY)  302 ENTERS THE FGD
SYSTEM.  THE FLUE GAS CONTACTS THE SCRUBBING SOLUTION THROUGH A SERIES OF SPRAY  ZONES ARRANGED VER-
TICALLY IN THE SPRAY TOWERS.  THE SCRUBBING MEDIUM IS A SOLUTION OF SOLUBILIZEO  ALKALI  (CAO, MGO,
NA20) OBTAINED FROM THE FLY ASH COLLECTED IN THE ESP'S, SUPPLEMENTED BY A LIME REAGENT, WHICH  IS
ADDED TO THE SOLUTION FOR S02 REMOVAL AND PH CONTROL PURPOSES.  BASED ON THE MAXIMUM  302  INLET CON-
CENTRATION AND THE REQUIRED NEW SOURCE EMISSION STANDARD OF 1.2 LB/MM BTU, THE ABSORBERS  REMOVE
APPROXIMATELY 85 PERCENT OF THE INLET S02.  BECAUSE 85 PERCENT OF THE FLUE GAS STREAM IS  TREATED,
THIS PRODUCES A TOTAL REMOVAL EFFICIENCY OF APPROXIMATELY 70 PERCENT AND RESULTS IN AN OUTLET  302
CONCENTRATION OF 535 PPM (DRY).  WHEN THE BOILER FIRES COAL WITH MAXIMUM SULFUR CONTENT (1.3X), THE
FGD SYSTEM OPERATES AT A LIQUID TO GAS (L/G) RATIO OF 80 IN THE SPRAY TOWERS; THE PH  AND  SUSPENDED
SOLIDS LEVELS IN THE RECYCLE SOLUTION AWE 6.4 TO 6.5 AND 12 PERCENT, RESPECTIVELY; AND SUPPLEMENTAL
LIME IS ADDED TO THE SYSTEM AT A RATE OF 4 TONS/HR.

     AFTER THE SCRUBBED GASES PASS THROUGH THE SPRAY ZONE OF THE ABSORBERS,  THEY ENTER A  CHEVRON-
TYPE MIST ELIMINATOR (ME).  A WASH TRAY, LOCATED BENEATH THE ME,  DILUTES ANY ENTRAINMENT  CARRIED
INTO THE ME TO PREVENT PLUGGING, SCALING, AND EVENTUAL RESTRICTION OF GAS FLOW.  THE  WASH TRAY OPER-
ATES OFF A SEPARATE REC1RCULATION LOOP AND TANK TO INSURE  A HIGH-QUALITY WASH WATER  LOW  IN SUSPEND-
ED SOLIDS AND DISSOLVED SALTS.  TO PREVENT PLUGGING, SPRAYS IRRIGATE THE ME'S WITH A  MIXTURE OF
MAKEUP WATER AND CLARIFIED LIQUOR FROM THE TRAY LOOP.  ALSO, SPRAYS UNDER THE WASH TRAY FLOOD  THE
UNDERSIDE OF THE TRAY AND THE AREA FROM THE TRAY DOWN TO THE TOP RECYCLE SPRAYS.

     THE SCRUBBED GAS STREAM IS REHEATED BY MIXING IT WITH THE 340 F 15 PERCENT BYPASS FLUE GAS
STREAM.  THIS RAISES THE TEMPERATURE OF THE SATURATED SCRUBBED GAS STREAM FROM 13b TO 165 F.   THE
GASES ARE THEN DISCHARGED TO THE ATMOSPHERE THROUGH THE STACK.  THE SPENT SCRUBBING SOLUTION IS DIS-
CHARGED TO A RECYCLE TANK AT THE BOTTOM OF THE  SPRAY TOWERS,  WHERE THE CHEMICAL
REACTIONS ARE COMPLETED.  FLUE GAS CLEANING WASTES (ALKALI SULFITE/SULFATE SALTS, FLY ASH) ARE DIS-
CHARGED FROM THE RECIRCULATION LOOP TO A THICKENER, WHERE THE WASTE SOLIDS SETTLE OUT.  THE CLARI-
FIED OVERFLOW FROM THE THICKENER IS RETURNED TO THE PROCESS AND USED FOR FLY ASH SLURRY PREPARATION.
THE THICKENER UNDERFLOW (MAXIMUM 40 PERCENT SOLIDS CONTENT) IS DISCHARGED TO A VACUUM THICKENER
BUILDING, WHICH HOUSES TWO ROTARY-DRUM VACUUM FILTERS FOR ADDITIONAL SOLIDS DEWATERING.   THE FILTER
CAKE, WHICH is PRODUCED AT A RATE OF 50 TONS/HR AND CONTAINS &o PERCENT SOLIDS, is TRANSPORTED BY
CONVEYOR TO THREE 35 TON, OFF-THE-ROAD TRUCKS FOR CONTINUOS HAULING TO A MINE LANDFILL RECLAMATION
AREA FOR FINAL DISPOSAL.  ADDITIONAL WATER RECOVERED IN THE VACUUM FILTER PROCESS IS  ALSO USED FOR
FLY ASH SLURRY PREPARATION.  DURING EMERGENCY CONDITIONS (MECHANICAL MALFUNCTION, HIGH FLOW RATES),
THE SLUDGE FROM THE VACUUM FILTER SYSTEM CAN BE PILED OUTSIDE THE VACUUM FILTER BUILDING  FOR HANDL-
ING BY FRONT END LOADERS AND OFF THE ROAD TRUCKS.
                                                  82

-------
MINNKOTA POWER COOPERATIVE                                        MILTON  R.  YOUNG  NO.  2

•INITIAL OPERATING EXPERIENCE*

     THE OPERATING UTILITY COMPANY HAS  REPORTED  INTERMITTENT  OPERATION  SINCE  INITIAL  START-UP  IN
SEPTEMBER 1977.  MAJOR OPERATIONAL PROBLEMS  HAVE  OCCURRED  AS  A  RESULT  OF SEVERE WINTER  WEATHER
CONDITIONS. PARTICULARLY NUMEROUS  INSTANCES  OF FROZEN  AND  RUPTURED  LINES.   THE  SYSTEM HAS  SHUT  DOWN
DURING THE FIRST PART OF THE MONTH OF DECEMBER TO INSTALL  HEAT  TRACING  IN  THE  LIQUID  CIRCUIT.   IN
ADDITION, SOME MINOR PROBLEMS  HAVE BEEN REPORTED  WITH  THE  SYSTEM'S  GUILLOTINE  GAS DAMPERS  AND  FLOW
METERS  (ROTAMETERS).

OCTOBER-NOVEMBER 1977 -  THE OPERATING UTILITY  COMPANY  WAS  REPORTED  INTERMITTENT OPERATION  SINCE
INITIAL  START-UP IN SEPTEMBER.   SEVERE  WINTER  WEATHER  PROBLEMS  HAVE CAUSED  FROZEN AND RUP-
TURED LINES.   THESE CONDTIONS  HAVE MADE SHUTDOWNS  NECESSARY  FOR  THE INSTALLATION OF  ELECTRICAL HEAT
TRACING  ON SLURRY  LINES  AND WATER  PIPING.

DECEMBER-JANUARY 1978 -  THERE  WAS  AN  EMER6ENCY SHUTDOWN ON DECEMBER 5  AS A  RESULT OF  BEARING  DAMAGE
WITHIN  THE TURBINES.  AS A CONSEQUENCE, THE  COMPLIANCE TEST ORIGINALLY  SCHEDULED  TO  dE  WITHIN  THIS
PERIOD  HAS BEEN  TENTATIVELY RESCHEDULED WITH THE  EPA FOR THE  END  OF MARCH.   THE UNIT  IS EXPECTED  TO
BE  BACK  ON LINE  FEB. 20  AT WHICH TIME THE  UTILITY EXPECTS  TO  HAVE THE  SYSTEMS  IN  EQUILIBRIUM  (WATER
BALANCE) .
                                                    83

-------
                  TABLE 3
PERFORMANCE DESCRIPTION FOR OPERATIONAL FGD SYSTEMS THROUGH
                                      01/78
 UTILITY NAME

 UNIT NAME

 UNIT LOCATION

 UNIT RATING

 FUEL CHARACTERISTICS

 FGD VENDOR

 PROCESS

 NEW OR RETROFIT

 START UP DATE

 FGD STATUS

 EFFICIENCY,
  PARTICULATES
MONTANA POWER CO.

COLSTRIP NO 1

COLSTRIP MONTANA

 360 MW

COAL 0.6 PERCENT SULFUR

ADL/COMBUSTION EQUIP ASSOCIATE

LIME/ALKALINE FLYASH SCRUBBING

NEW

11/75

OPERATIONAL


99.5 PERCENT  ACTUAL
  S0£


 WATER MAKE UP
70-75 PERCENT (ACTUAL)
                       CLOSED LOOP
 SLUDGE DISPOSAL
                       CLAY-LINED DIKED POND
 UNIT COST
                      SEE APPENDIX A, FGD SYSTEM ECONOMICS
 OPERATIONAL
  EXPERIENCE
REFER TO THE BACKGROUND INFORMATION SECTION IN TABLE 3 OF THIS  REPORT.
THIS FGD EQUIPPED UNIT WAS DECLARED COMMERCIAL IN NOVEMBER  1975.   THE
SCRUBBING SYSTEM PROVIDES PARTICULATE AND S03 CONTROL WITH  THREE  SCRUB-
BER MODULES.  EACH MODULE CONSISTS OF A DOWNFLOW VENTURI SCRUBBER  CENTER-
ED WITHIN AN UPFLOW SPRAY TOWER ABSORBER.  EACH MODULE CAN  TREAT  10X OF
THE TOTAL BOILER FLUE GAS AND THE MODULES CANNOT BE BYPASSED.   THE  UN-
STABILIZED SLUDGE IS DISPOSED IN AN ON-SITE LINED DISPOSAL  POND.   IN-LINE
STEAM REHEAT AND CLOSED WATER LOOP CAPABILITY ARE INCLUDED  IN THE  SYSTEM.
                                                84

-------
                  TABLE 3
PERFORMANCE DESCRIPTION FOR OPERATIONAL  FGO  SYSTEMS  THROUGH
                                       01/78
 UTILITY NAME

 UNIT NAME

 UNIT LOCATION

 UNIT RATING

 FUEL CHARACTERISTICS

 FGD VENDOR

 PROCESS

 NEW OR RETROFIT

 START UP DATE

 FGO STATUS

 EFFICIENCY,
   PARTICULATES
 MONTANA  POWER  CO.

 COLSTRIP NO 2

 COLSTRIP MONTANA

  360  MW

 COAL  0.8 PERCENT SULFUR

 AOL/COMBUSTION EQUIP ASSOCIATE

 LIME/ALKALINE  FLYASH SCRUBBING

 NEW

  7/76

 OPERATIONAL


 99.5  PERCENT  ACTUAL
   soa
 70-75 PERCENT (ACTUAL)
  WATER  MAKE  UP
 CLOSED LOOP
  SLUDGE  DISPOSAL
  UNIT  COST
SEE APPENDIX A, FGO SYSTEM ECONOMICS
  OPERATIONAL
   EXPERIENCE
 REFER TO THE BACKGROUND INFORMATION SECTION IN TABLE 3 OF THIS REPORT.
 THIS FGD EQUIPPED UNIT WAS DECLARED COMMERCIAL IN AUGUST 1976.  THE
 SCRUBBING SYSTEM PROVIDES PARTICULATE AND S02 CONTROL WITH THREE SCRUB-
 BER MODULES.  EACH MODULE CONSISTS OF A DOWNFLOW VENTURI SCRUBBER CENTER-
 ED WITHIN AN UPFLOW SPRAY TOWER ABSORBER.  EACH MODULE CAN TREAT 70X OF
 THE TOTAL BOILER FLUE GAS AND THE MODULES CANNOT BE BYPASSED.  THE UN-
 STABILIZEO SLUDGE IS DISPOSED IN AN ON-SITE LINED DISPOSAL POND.  IN-LINE
 STEAM REHEAT AND CLOSED WATER LOOP CAPABILITY ARE INCLUDED IN THE SYSTEM.
                                                85

-------
                                       BACKGROUND INFORMATION
                                                 UN
                                       COLSTRIP UNITS 1 AND 2

     THE COLSTRIP POWER STATION OF THE MONTANA POWER COMPANY 13 LOCATED  NEAR  COLSTRIP.  MONTANA,
APPROXIMATELY 100 MILES EAST OF BILLINGS, MONTANA. THE STATION CONTAINS  TWO NEW  360-MW  COAL-FIRED
POWER-GENERATING UNITS.  AT THE PRESENT TIME, THE UTILITY IS PLANNING  THE  ADDITION  OF  TWO MORE
700-MW COAL-FIRED POWER-GENERATING UNITS AT THE STATION.  THIS MINE MOUTH  PLANT  FIRES  LOW-SULFUR,
LOW HEAT CONTENT COLSTRIP COAL, PRODUCING A FLUE GAS CONTAINING UP TO  6  GR/SCFD  PARTICULATE AND UP
TO 1000 PPM SULFUR DIOXIDE.  THE GENERAL CHARACTERISTICS OF THIS COAL  ARE;  HEATING VALUE (AS FIRED)
68«3 BTU/LB. (MIN. 6162 BTU/LB); SULFUR CONTENT, 0.77 PERCENT (12 MAX);  ASH CONTENT,  8.59 PERCENT;
MOISTURE CONTENT, 23.87 PERCENT.

     IN ORDER TO MEET AIR POLLUTION EMISSION STANDARDS OF 400 PPM FOR  SULFUR  DIOXIDE  (1.0 LB/MM BTU)
AND 0.03 GR/SCFD FOR PARTICULATES, THE BOILERS ARE EQUIPPED WITH SCRUBBER  PLANTS FOR  THE CONTROL OF
PARTICULATES AND SULFUR DIOXIDE.  THE SYSTEMS INSTALLED ON UNITS 1 AND 2 WERE DESIGNED  AND SUPPLIED
BY COMBUSTION EQUIPMENT ASSOCIATES (CEA) AND AUTHUR D. LITTLE (ADD.   THE  PROCESS INSTALLED UTILIZES
THE HIGH ALKALINITY OF THE FLY ASH (APPROXIMATELY 20 PERCENT CALCIUM OXIDE) FOR  THE REMOVAL OF
SULFUR DIOXIDE AND SUPPLEMENTAL LIME SLURRY FOR PH AND SCALE CONTROL.  DESIGN PARTICULATE AND SULFUR
DIOXIDE REMOVAL EFFICIENCIES ARE 99.5 AND 60 PERCENT, RESPECTIVELY.

     EACH BOILER IS EQUIPPED WITH THREE SCRUBBER MODULES, EACH MODULE  CAPABLE OF HANDLING HO PERCENT
OF THE BOILER FLUE GAS CAPACITY (1,430,000 ACFM AT 291F).  EACH SCRUBBER INCORPORATES  A VARIABLE-
THROAT VENTURI (DESIGN SUPERFICIAL GAS VELOCITY; 200 FT/SEC), A SPRAY  ABSORPTION SECTION (DESIGN
SUPERFICIAL GAS VELOCITY; 11.5 FT/SEC), AN INTERNAL RECYCLE TANK, A WASH TRAY, AND  A CHEVRON-TYPE
MIST ELIMINATOR.  THE VENTURI AND SPRAY SECTIONS OPERATE ON A RECIRCULATING SLURRY  LOOP CONTAINING
12 PERCENT SOLIDS (CONSISTING PRIMARILY OF CALCIUM SALTS AND FLY ASH).   TOTAL MODULE PRESSURE DROP
IS APPROXIMATELY 23.5 INCHES H20. TOTAL MODULE LIQUID-TO-GAS RATIO IS  APPROXIMATELY 33  GAL/1000 ACF.
A WASH TRAY IS SITUATED BENEATH THE MIST ELIMINATOR IN ORDER TO DILUTE ANY ENTRAINMENT  REACHING THE
COMPONENT, THUS REDUCING THE POTENTIAL FOR PLUGGING AND SCALING.  THE  TRAY OPERATES OFF A SEPARATE
RECYCLE TANK AND RECIRCULATION LOOP.  REHEAT IS SUPPLIED BY IN-THE-FLUE-GAS-STREAM  STEAM TUBE BUND-
LES (MINIMUM DELTA T: 50F).  THE REHEATERS ARE ALSO EQUIPPED WITH SOOT BLOWERS FOR  CLEANING.  THE
SCRUBBER BOOSTER FANS (INCLUDED DRAFT, 43.5 INCHES H20) ARE LOCATED DOWNSTREAM OF THE SCRUBBERS AND
OPERATE ON DRY, REHEATED FLUE GAS.  THE FANS WERE LOCATED DOWNSTREAM IN  THIS  SCRUBBER DESIGN BECAUSE
OF THE HIGH PARTICULATE LOADING OF THE INLET FLUE GAS.  THE SCRUBBING WASTES  (UNREACTED FLY  ASH,
9 PARTS CALCIUM SULFATE/1 PART CALCIUM SULFITE) ARE DISCHARGED TO AN INITAL HOLDING BASIN (520 ACRE-
FEET) ADJACENT TO THE SCRUBBER PLANT AND THEN PUMPED (50.8 DRY TPH/2 UNITS) THREE MILES TO A PERMAN-
ENT SLUDGE DISPOSAL POND (2218 ACRE-FEET, CLAY-LINED WHERE NECESSARY).  CLEAN  LIQUOR IS RETURNED
FROM PONDS FOR ADDITIONAL SCRUBBING SERVICE.  FRESH MAKE-UP WATER TO THE SYSTEM  IS  LIMITED TO AP-
PROXIMATELY THE AMOUNT OF WATER LOST IN THE SCRUB BER PLANT VIA EVAPORATION AND  SLUDGE.

PERFORMANCE HISTORY:

UNIT NO. 1 BECAME AVAILABLE FOR SERVICE DURING THE LATTER PART OF 1975.  UNIT  NO. 2 WAS PLACED IN
SERVICE DURING THE SUMMER OF 1976.  THE OVERALL PERFORMANCE OF THE SCRUBBER SYSTEM  HAS  BEEN  EXCELL-
ENT, HOWEVER, THE OPERATIONAL EXPERIENCE OF THESE FULL SCALE UNITS HAS SHOWN  SEVERAL PROBLEM AREAS.
INSTRUMENTATION IN SLURRY AND FLUE GAS SERVICE HAS NOT BEEN TROUBLE FREE.  THE STACK OPACITY, S02
AND N03 MONITORS ALONG WITH 302 MONITORS ON THE   INLET AND THE OUTLET OF  THE  SCRUBBER  MODULES HAVE
EXHIBITED UNSTABLE AND ERRATIC BEHAVIOR.  IN-LINE  PH PROBES HAVE EITHER ERODED  AWAY OR LOST SENSI-
TIVITY DUE TO DEPOSITS FORMING ON THE ELEMENTS.  MANUAL SAMPLING IS REQUIRED  FOR CHEMICAL CONTROL OF
THE PH AS WELL AS THE SLURRY DENSITY.  WET-DRY DEPOSITS HAVE FORMED AT THE INLET TO THE SCRUBBER
VESSEL WHERE THE HOT, DUST-LADEN GAS IS COOLED AND HUMIDIFIED. THESE DEPOSITS, NOT  TO BE CONFUSED
WITH CALCIUM SULFATE SCALE, REQUIRE MANUAL REMOVAL FROM EACH SCRUBBER MODULE  EVERY  TWO  WEEKS.  LAB-
ORATORY MODEL TESTS ON GAS FLOW AND LIQUID DISTRIBUTION PLUS FULL SCALE TESTS  IN ONE SCRUBBER MODULE
WHICH INVOLVE BOTH LIQUID AND GAS FLOW TURNING VANES SHOW PROMISE IN EXTENDING THE  TIME BETWEEN
CLEANINGS.  IN VIEW OF THE PROMISING RESULTS, THESE MODIFICATIONS ARE BEING INSTALLED ON ALL THREE
MODULES OF UNIT NO. i.

THE SUPPLEMENTARY ALKALI FEED PROVIDED BY THE LIME SYSTEM IS REQUIRED FOR  EFFECTIVE CHEMICAL CONTROL
OF THE SCRUBBER SYSTEM.  PLUGGING OF LINES AND EQUIPMENT FAILURE HAVE MADE THE LIME SYSTEM DIFFICULT
TO USE, THE ALKALI FOUND IN THE ASH WHICH IS CAPTURED BY THE SCRUBBER HAS  BEEN GENERALLY ADEQUATE
TO KEEP THE PH WITHIN THE CONTROL RANGE.  BETTER CONTROL OF THE LIME SYSTEM WOULD KEEP  THE PH MORE
CONSTANT AND ALLOW THE S02 REMOVAL TO BE OPTIMIZED.  FAILURES OF THE PROTECTIVE  GLASS-FLAKE  LINING
OVER THE CARBON STEEL VESSEL WALLS AND DUCTS HAS OCCURRED IN SEVERAL AREAS.   THESE  FAILURES  WERE
EVIDENT PRIOR TO A MAJOR TEMPERATURt EXCURSION THAT OCCURRED ON UNIT NO. 1 IN  OCTOBER  1976.   THE
TEMPERATURE EXCURSION FOLLOWED A STATION BLACKOUT AND THE FAILURE OF THE EMERGENCY  SCRUBBER  QUENCH
WATER SUPPLY SYSTEM TO OPERATE.  GLASS-FLAKE LINING AND PLASTIC CHEVRON MIST  ELIMINATORS WERE DAM-
AGED AT THAT TIME AND ACCOUNT FOR THE LOW SCRUBBER AVAILABILITY DURING NOVEMBER  AND DECEMBER
A FAILURE OF AN ID FAN MOTOR DURING THE SAME TIME PERIOD INDEPENDENT OF  THE TEMPERATURE EXCURSION
ALSO CONTRIBUTED TO THE LOWER AVAILABILITY FIGURE.  QUICK CLEAN BASKET STRAINERS WERE  ADDED  TO THE
SUCTION PIPING OF THE TwO MAIN RECYCLE PUMPS OF EACH VESSEL TO REMOVE FOREIGN  MATERTAIS ANn  HFPnSTTS
BEFORE THE* CLOG SPRAY NOZZLES.                                                              ucruoi

     A PROGRAM IS UNDER WAY TO EVALUATE ABRASION RESISTANT PROTECTIVE LINING  MATERIALS  THAT  fOULD BE
USED WHERE THE FLUE GAS MAKES ITS 180 DEGREE TURN FOLLOWING THE VENTURI DOWN-COMER  ANn  PASSFS HYTHF
ABSORPTION SPRAYS.                                                                      r.oota 01

     ADDITIONAL INFORMATION CONCERNING THE PERFORMANCE OF THE COLSTRIP FGD SYSTEM MOOULFS IS TNr-
LUDEO IN THE FOLLOWING TABLE.  A GENERAL PROCESS FLOW DIAGRAM OF THE SCRUBBING SYSTFM  IS
IN APPENDIX B.
                                                  86

-------
MONTANA POWER CO.
                                                                 COLSTKIP UNIT NOS. 1  AND 2
      NOTE: SCRUBBER AVAILABILITY  IS  DEFINED  BY  MONTANA POWER AS THE TOTAL MODULE HOURS AVAILABLE
            DIVIDED BY  THREE  TIMES  THE  HOURS  IN  THE  MONTH (BECAUSE THERE ARE THREE SCRUBBER MODULES
            PER GENERATING UNIT) AND  EXPRESSED AS  A  PERCENTAGE.  WHENEVER WORK IS DONE ON A MODULE
            THAT TAKES  IT OUT  OF SERVICE  OR WOULD  PREVENT ITS USE (rtHETHER THE BOILER IS OPERATING
            OR NOT), THE RESPECTED  MODULE IS  TERMED  UNAVAILABLE.
          MONTHLY CAPACITY
              FACTOR X
UNIT
SEP. 75
OCT. 75
NOV. 75
DEC. 75
JAN. 76
FEB. 76
MAR. 76
APR. 76
MAY 76
JUN. 76
JUL. 76
AUG. 76
SEP. 76
OCT. 76
NOV. 76
DEC. 76
JAN. 77
FEB. 77
MAR. 77
APR. 77
MAY 77
JUN. 77
JUL. 77
AUG. 77
SEP. 77
OCT. 77
NOV. 77
DEC. 77
1
1
19
42
60
64
65
57
50
26
0
28
38
65
73
56
67
73
3
0
50
64
69
72





2








1
23
20
13
65
77
80
82
68
75
71
68
£3
61
58





*UNIT NO. 2 AVAIL


OUTAGE. SCR
IS THE AVAIL
UBBE
ABIL
NO.
ON
1
3
19
24
30
26
24
28
14
0
20
23
30
30
30
31
31
2
0
25
26
28
29
DAYS
LINE
2







3
16
13
10
30
31
30
31
30
27
28
29
13
28
28
AVG

   1
  50
 139
 203
 239
 265
 273
 277
 219
 210
   0
 167
 194
 239
 281
 225
 249
 270
 161

 23fa
 286
 284
 284
                                                               ON
FOR DAYS
LINE
    2
                                                                     66
                                                                    171
                                                                    180
                                                                    162
                                                                    232
                                                                    298
                                                                    303
                                                                    297
                                                                    258
                                                                    285
                                                                    293
                                                                    264
                                                                    209
                                                                    249
                                                                    238
   SCRUBBER
AVAILABILITY X
90
98
98
74
97
 0
93
95
89
80
63
74
93
95
                         1ILITY OF 77X FOR OCTOBtH 1977 INCLUDES NO
                          MAINTENANCE WAS PERFORMED THROUGH PART OF
                         n NOT INCLUDING THE BOILER OUTAGE TIME.
         AVAILABLE HOURS
         THE OUTAGE TIME
                              100
                              100
                               99
                               96
                               98
                               90
                               94
                               93
                               83
                               94
                               97
                    83         85
                    85         63
                    87         88
                    85         91
                    93         81
                    93         90
                    96         77*
                               98*
                    96         98
                    98         98
                  DURING A BOILER
                 ,   THE 98X FIGURE
                                                    87

-------
                  TABLE 3
PERFORMANCE DESCRIPTION FOR OPERATIONAL FGD SYSTEMS  THROUGH   01/78
 UTILITY NAME


 UNIT NAME


 UNIT LOCATION


 UNIT RATING
NEVADA


REID GARDNER UO 1


MOAPA NEVADA


 125 MW
 FUEL CHARACTERISTICS  COAL O.b - 1.0 PERCENT SULFUR
 FGD VENDOR


 PROCESS


 NEW OR RETROFIT


 START UP DATE


 FGD STATUS


 EFFICIENCY,
  PARTICULATES
AOL/COMBUSTION EQUIP ASSOCIATE


SODIUM CARBONATE SCRUBBING


RETROFIT


 H/T*


OPERATIONAL



99 PERCENT
  S02
                       85 PERCEfJT
 MATER MAKE UP
                       OPEN LOOP 0.4U GPM/MW
 SLUDGE DISPOSAL
                       SOLAR EVAPORATION POND
 UNIT COST
                      SEE APPENDIX A, FGD SYSTEM ECONOMICS
 OPERATIONAL
  EXPERIENCE
REFER TO THE BACKGROUND I NFORrtA T ION SECTION IN TABLE  3 OF  THIS  REPORT.
THIS SODIUM CAR60i\iATE-6ASED (TRONA) SCRUBBING SYS1EM  CONSISTS OF  ONE
MODULE CONTAINING A TuIN VARIABLE-THROAT VENTURI SCRUBBER  FOLLOWED  BY  A
SEPARATOR IN StKlES rtlTH A SINGLE-STAGE PERFORATED-PLATE A8SOHBEH  TOWER.
PRIMARY PAHTICULATt CONTROL IS PROVIDED BY UPSTREAM MECHANICAL  COLLECTORS.
A STEAM INDIRECT HOT AlK REHEAT SYSTEM RAISES THE GAS TEMPERATURE  30 F
PRIOR TO DISCHARGE TO TrlE MAIN STACK. THE FLUE GAS CLEANING  WASTES  ARE
ULTIMATELY DISPOSED IN AN ON-SITE CLAY-LINED SOLAR EVAPORATION  POND.
                                               88

-------
                                       BACKGROUND  INFORMATION
                                                 ON
                                  REID GARDNER UNITS  1,  2,  AND  3

     THE  REID GARDNER POWER STATION IS LOCATED NEAR MOAPA,  NEVADA,  ABOUT  50  MILES  NORTH  OF  LAS  VEGAS
THE STATION HAS THREE ELECTRIC POWER GENERATING UNITS,  (REIO GARDNER  1, 2, AND  3)  EACH RATED  AT
125 MW.   UNITS 1 AND 2 ARE RETROFITTED WITH SODIUM CAR86NATE-BASEO  FGO  SYSTEMS.  UNIT NO. 3 IS  A NEW
INSTALLATION, ALSO EQUIPPED WITH A SODIUM CARBONATE-BASED  FGD SYSTEM.   THE COAL  BURNED AT THE PLANT
HAS AN AVERAGE GROSS HEATING VALUE OF 12,450 BTU/L8.   AND  ASH AND SULFUR  CONTENTS  OF 8 AND  0.5
PERCENT  RESPECTIVELY.

     THE FGD SYSTEMS INSTALLED ON REID GARDNER UNITS  1,2,&3 WERE DESIGNED AND  INSTALLED  BY  COM-
BUSTION EQUIPMENT ASSOCIATES IN ASSOCIATION WITH A. D.  LITTLE.   THE SYSTEMS  FOR  UNITS 1  AND 2 WERE
PLACED IN SERVICE IN APRIL 1971.  THE SYSTEM FOR UNIT  3 WAS PLACED  IN OPERATION  ON JULY  12, 1976.
THE SCRUBBING SYSTEM DESIGN WAS BASED ON  INFORMATION  AND DATA OBTAINED  FROM  AN  8000-ACFM PILOT  PLANT
PROGRAM CONDUCTED AT THIS STATION IN 1971 AND  1972.

     THE FGD SYSTEM CONSISTS OF A SINGLE  MODULE, DESIGNED  TO HANDLE 473,000  ACFM OF GAS  AT  350  F.
THE MODULE IS MADE UP OF A TWIN VARIABLE-THROAT VENTURI SCRUBBER, FOLLOWED BY  A  SINGLE-STAGE  TRAY
TOWER ABSORBER.  GAS BYPASS IS ACHIEVED BY A GUILLOTINE-TYPE DAMPER.  A COMMON  FACILITY  FOR TRONA
(SODIUM CARBONATE ORE) STORAGE AND SAND REMOVAL SERVES  ALL  THE  FGO  MODULES AT  THE  REID GARDNER
PLANT.  SULFUR DIOXIDE REMOVAL EFFICIENCY is REPORTED  TU BE as  PERCENT.   PRIMARY PARTICULATE  REMOVAL
IS ACCOMPLISHED BY 75 PERCENT EFFICIENT MECHANICAL COLLECTORS INSTALLED UPSTREAM OF THE  WET SCRUB-
BERS.  THE TOTAL PARTICULATE REMOVAL EFFICIENCY OF THE  MECHANICAL COLLECTION AND WET SCRUBBING
SYSTEM EXCEEDS  THE 99 PERCENT LEVEL.

      IN THIS SODIUM CARBONATE PROCESS, HOT FLUE GAS FROM THE BOILER PASSES FIRST THROUGH THE  MECHAN-
ICAL COLLECTORS WHERE PRIMARY PARTICULATE REMOVAL  TAKES PLACE.   PRESSURE  IS  THEN BOOSTED BY AN  IND-
UCED DRAFT FAN  BEFORE THE GAS STREAM SPLITS AS IT  ENTERS THE TWIN-THROAT  VENTURI SCRUBBER.  THE HOT
FLUE GAS  IS  QUENCHED BY  A SHOWER OF CIRCULATED SODIUM-BASE  LIQUOR.   THE GAS  THEN tNTERS  THE TRAY
TOWER AND  BUBBLES THROUGH THE RADIAL-VANE MIST ELIMINATOR,  WHERE THE  REMAINING  LIQUID DROPLETS  CAR-
RIED OVER  WITH  THE GAS ARE TRAPPED AND REMOVED.

     EFFLUENT FROM THE FGD SYSTEM IS FROM TWO  SOURCES:   THE SLIP STREAM OF SPENT LIQUOR  DISCHARGED
FROM  THE  RECIRCULATION TANK, AND THE ALKALINE  CLAHIFIER UNDERFLOW,  WHICH  SERVES  TO NEUTRALIZE THE PH
OF  THE COMBINED LIQUOR BEFORE IT IS DISCHARGED TO  THE  SLUDGE SETTLING PONDS.  THE  SPENT  LIQUOR  IS
PUMPED INTO  ONE OF TWO SETTLING PONDS.   THE OVEKFLOW  FROM  THIS  POND IS  PUMPED  TO A LARGER 45-ACRE
POND, WHERE  THE BRINE IS EVAPORATED.  THE FGD  SYSTEM  OPERATES ON AN OPEN  WATER  LOOP WITH NO LIQUOR
RECYCLED  TO  THE MODULES  FROM THE PONDS.

      ADDITIONAL INFORMATION CONCERNING THE PEHFORMANCt  OF  THE SCRUBBERS INSTALLED  AT THE REID
GARDNER STATION,  INCLUDING PROBLEMS, SOLUTIONS, AND MODIFICATIONS,  ARE  PRESENTED IN THE  FOLLOWING
TABLES.   IN  ADDITION, A  GENERAL PROCESS  FLOW DIAGRAM  OF THE SODIUM  CARBONATE SCRUBBING SYSTEM IS
PRESENTED IN APPENDIX 8.

-------
NEVADA POWER                                                          REID  GARDNER UNIT NO. 1

                                             HR.
                  BORER       MODULE      CALLtO
           TOTAL OPERATION   AVAILABLE     UPON TO   OPERATION
PERIOD     (HR.)   (HR.)       IHR.)       OPERATE      (HR.)
MAR. 75
APR. 75
MAY  75
JUN. 75
       DURING FEBRUARY THE FGD SYSTEM OPERATED KITH 95 PERCENT AVAILABILITY  ON  TRONA  SUPPLEMENTED
       WITH SODA ASH.  AVAILABILITY IN JANUARY HAS ONLY ABOUT 65 PERCENT BECAUSE  OF  FROZEN SODIUM
       CARBONATE FEED LINES.  PROBLEMS IN FEBRUARY INCLUDED A 2-DAY LACK OF  CHEMICALS.  NO SIGNIFI-
       CANT PROBLEMS OCCURRED IN MARCH.  THE UNIT RAN APRIL 1 THROUGH  APRIL  12  WITH  100 PERCENT
       AVAILABILITY.  THE BOILER WAS THEN SHUT DOWN FUR ROUTINE MAINTENANCE.   THE SYSTEM WAS PLACED
       BACK ON LINE MAY 12.  SECOND PERFORMANCE TEST WAS PASSED.  PROBLEMS  INCLUDED  ABRASION OF
       RUBBER-LINED PIPES AND ROUTINE MECHANICAL AND INSTRUMENTAL PROBLEMS.   HIGH ASH CONTENT,  UP TO
       20 PERCENT, HAD NO EFFECT ON EMISSIONS.  OPERABILITY FOR THE MONTH  OF  JULY WAS 85 PERCENT.

JUL. 75
AUG. 75
SEP. 75    720     716                                  559
OPERABILITY s 78X
UTILIZATION = 7ttX
       OF THE 4 OUTAGES REPORTED, 3 WERE CAUSED BY SCRUBBER MALFUNCTIONS.

OCT. 75    744     303                                  106
OPERABILITY = 60X
UTILIZATION = 141
       LOW OPERATING TIME WAS DUE TO SCHEDULED BOILER MAINTENANCE.  ONE OUTAGE  WAS DUE TO THE MAL-
       FUNCTION OF A SODA ASH BLOWER.

NOV. 75    720      654                                 394
OPERABILITY s 60X
UTILIZATION = 55X
       THE UTILITY REPORTS SYSTtM PERFORMANCE IN TERMS OF THE OPERABILITY  INDEX.  UNIT  NO.  1 OPER-
       ABILITY WAS LOW FOR 1HE MONTH OF NOVEMBER BECAUSE OF DELAYS IN DELIVERY  OF REPAIR MATERIALS.
       THREE FORCED OUTAGES DURING THE MONTH WERE DUE TO REHEATER STEAM LEAKS,  COLLAPSE  OF  A VENTURI
       STRAINER, AND A FROZEN CARBONATE LINE.  THE SYSTEM WAS SHUT DOWN FOR 16  DAYS FOR  COMPLETION
       OF PIPING CONVERSION: THIS OUTAGE WAS NOT DUE TO SCRUBBER MALFUNCTION.

DEC. 75
JAN. 76    744      647         604          327        186
AVAILABILITY = 81X
OPERA8ILITY = 29X
RELIABILITY = 57X
UTILIZATION = 25X

FEB. 76    6*6      664         631          585        520
AVAILABILITY = 91X
OPERABILITY = 78X
RELIABILITY = 89X
UTILIZATION = 75X
       THE UTILITY REPORTED FIVE SCRUBBER INOPERATIVE PERIODS DURING THE MONTH  OF FEBRUARY,  TWO  OF
       WHICH WERE SCRUBBER RELATED OUTAGES.  THE FORCED SCRUBBER OUTAGES OCCURRED BECAUSE  OF A
       DEPLETION OF CHEMICAL, CHEMICAL LINE PLUGGING AND SEAL WATER PROBLEMS.

MAR. 76    744      398         743          288        287
AVAILABILITY = 99X
OPERABILITY = 72X
RELIABILITY = 99X
UTILIZATION = 39X
       ONLY ONE FORCED SCRUBBER OUTAGE OCCURRED DURING THE MONTH BECAUSE OF A VENTURI  LEAK.

APR. 76    720      106         106          97         97
AVAILABILITY = 15X
OPERAblLITY = 91X
RELIABILITY = 100X
UTILIZATION = 13*
       THE BOILER WAS TAKEN OUT OF SERVICE APRIL 5 FOR INSPECTION OF VALVES AND CUAL  CONDUITS.

MAY  76
JUN. 76
ALL INDEX VALUES = OX
       THE NO.  1  UNIT WAS SHUT DOWN THE ENTIRE MONTH fOX A SCHEDULED TURBINE OVERHAUL  AMD  BURNER
       LINE CONDUIT REPLACEMENT.                                                 t"n«uL  »wu  BUKNtK
                                                  90

-------
NEVADA POWER
                                                                  REID GARDNER UNIT NO. i
PERIOD
                  BOILER
           TOTAL OPERATION
           (MR.)   (MR.)
  MODULE
AVAILABLE
  (HR.)
  HR.
CALLED
UPON TO
OPERATE
OPERATION
  (HK.)
JUL. 76
ALL INDEX VALUES = OX
       THE NO. 1 UNIT REMAINED  OUT  OF  SERVICE THROUGHOUT THE MONTH FOR COMPLETION OF THE TURBINE AND
       BOILER OVERHAUL WHICH  COMMENCED THE PRfcCEEOING MONTH.
                    479
                                 719
                                              366
                                                         360
AUG.  76    744
AVAILABILITY = 971
OPERABILITY = 7SX
RELIABILITY = 94X
UTILIZATION = 49X
       TWO FORCED SCRUBBER OUTAGES OCCURRED  DURING  THE  MONTH  ATTRIBUTED  TO PLUGGING IN THE TRAY  RE-
       CYCLE TANK AND THICKENER TANK.   TOTAL  BOILER  OUTAGE  TIME  FUR  THE  MONTH EXCEEDED 265 HOURS.

SEP.  76    720      656         683           676         639
AVAILABILITY = 95X
OPERABILITY as 97X
RELIABILITY e 95X
UTILIZATION = 89X
       TWO FORCED SCRUBBER OUTAGES WERE  REPORTED  BY  THE  UTILITY  FOR  THE  MONTH.   THESE  MINOR OUTAGES
       WERE CAUSED BY PLUGGING IN THE  VENTURI  SPRAY  HEADERS AND  AN  i.e.  FAN MALFUNCTION.   TOTAL
       FORCED OUTAGE TIME AMOUNTED TO  36.8«  HOURS.

OCT.  76    744      678         728           664         648
AVAILABILITY = 98X
OPERABILITY = 96X
RELIABILITY » 98X
UTILIZATION = 87X
       SCRUBBER OUTAGE TIME WAS REQUIRED FOR  INSTALLATION OF  A  NEW  CARBONATE FEED  LINE.   IN
       ADDITION, A MINOR SCRUBBER TRIP WAS CAUSED BY PLUGGING IN THE SCRUBBER EFFLUENT SUCTION LINE,
                     631
                                 623
                                              605
                                                         508
 NOV.  76     720
 AVAILABILITY  =  87x
 RELIABILITY f 84X
 OPERABILITY = SIX
 UTILIZATION = 71X
       ONE  FORCED  SCRUBBER OUTAGE OCCURRED DURING THE REPORT PERIOD BECAUSE OF A SCREW CONVEYOR
       FAILURE,  RESULTING IN AN INABILITY TO MIX THE CHEMICAL ABSORBENT.
                                  690
                                              652
                                                         599
DEC. 76    744     677
AVAILABILITY = 93X
RELIABILITY = 92X
OPERABILITY = 88X
UTILIZATION = SOX
       TWO FORCED SCRUBBER OUTAGES  OCCURRED  DURING  DECEMBER  BECAUSE  OF  CHEMICAL  DEPLETION  AND  A
       PLUGGED SENSING LINE.
                                 533
                                              501
                                                         437
 JAN.  77     744      645
 AVAILABILITY  a  72X
 RELIABILITY = 87X
 OPERABILITY s 67X
 UTILIZATION = 59X
        THE  SCRUBBER OPERATED WITH NO DOWNTIME UNTIL JANUARY 22,  WHEN RUBBER LINING REPAIRS WERE
        INITIATED  IN THE SEPARATOR SECTION IN THE SCRUBBING MODULE.  THE SCRUBBER WAS DOWN THROUGHOUT
        THE  REST OF  THE REPORT PERIOD.
                                    0
                                              599
 FEB.  77     672      599
 ALL  INDEX  VALUES  =  OX
       SYSTEM SHUT  DOWN FOR CONTINUATION OF RUBBER LINING REPAIRS.
                                    0
                                              669
                                                           0
 MAR.  77     744      669
 ALL  INDEX  VALUES  =  OX
       SYSTEM SHUT  DOWN  FOR  CONTINUATION OF RUBBER LINING REPAIRS.

 APR.  77
 ALL  INOEX  VALUES  =  OX
       THE  MODULE WAS UNAVAILABLE FOR SERVICE DURING THE REPORT MONTHS BECAUSE OF REPAIRS TO THE
       SCRUBBER LINING DAMAGED  FROM A HIGH TEMPERATURE EXCURSION RESULTING FROM A MALFUNCTION IN THE
       UNIT'S AIR PREHEATER

 MAY   77
 ALL  INDEX  VALUES  =  OX
                                                   91

-------
NEVADA POWER                                                     KEIO  GARDNER  UNIT  NO.  1

                                             HR.
                  BOILER       MODULE      CALLED
           TOTAL OPERATION   AVAILABLE     UPON TO   OPERATION
PERIOD     (HR.)   (HR.)       (HR.)       OPERATE     (HR.)
JUN. 77    720      701        339          720        315
AVAILABILITY = 4?x
RELIABILITY = It*
OPERABILITY = 45X
UTILIZATION = 44X
       REPAIRS ON THE DAMAGED RUBBER LINING WEKt COMPLETED BY MID-JUNE AND  THE  SYSTEM REMAINED IN
       SERVICE THROUGHOUT THE MONTH WITH THE EXCEPTION OF ONE MINOR FORCED  OUTAGE  (7.5  MRS.  FOR A
       HIGH-LOW PRESSURE TRIP CAUSED bY A PLUGGED SENSING LINE).

JUL. 77    744      744        740          744        744
AVAILABILITY = 99%
StLIABILITY s 99X
OPERABILITY = S9X
UTILIZATION = 99X
       THE SYSTEM WAS TAKEN OUT OF 1 HE GAS PATH ONLY ONCE DURING THE MONTH  BECAUSE  OF A SCHEDULED
       INSPECTION OF THE NEWLY REPLACED RUBBER LINER IN THE SEPARATOR  SECTION.

AUG. 77    744      662        138          744        138
AVAILABILITY = 19X
RELIABILITY = 19X
OPERABILITY = 21X
UTILIZATION = 19X
       I.D. FAN RELAYS WERE INSTALLED BECAUSE OF HIGH FAN VIBRATIONS.

SEP. 77    720      343        720          720        252
AVAILABILITY = 64%
RtLIABILITY * 69*
OPERABILITY r 73X
UTILIZATION s 35X
       BOILER WAS OUT OF SERVICE FOR MOST Of THE MONTH.  BOILER RETURNED TO SERVICE ON  THE 2«TH.
       THE SCRUBBER STILL HAD LIMIT SWITCH PROBLEM WITH 14 A & B GUILLOTINE DAMPERS.

OCT. 77    744      635          630         744        630
AVAILABILITY = 99X
RELIABILITY s 99X
OPERABILITY = 99X
UTILIZATION = 84.7X
       THE UNIT WAS SHUT DOWN FOR 5 HOURS DURING OCTOBER TO REPAIR AN  ID FAN LEAK.  THE BALANCE Of
       THE OUTAGE TIME WAS BOILER RELATED.  (TOTAL OUTAGE TIME WAS 113.92 HOURS).

NOV. 77    720      690          693         589        562
AVAILABILITY s 78.7X
RtLIABILITY s 76.6X
OPERABILITY = 81.5X
UTILIZATION s 78.IX
       THE SCRUBBER WAS DOWN APPROXIMATELY 153.57 HRS. DURING NOVEMBER.  PROBLEMS ENCOUNTERED  IN-
       CLUDED SCREEN PLUGGING IN THE RECYCLE TANK AND A SCRUBBER INSTRUMENTATION DIFFICULTY.   THE
       SYSTEM WAS ALSO DOWN FOR THE INSTALLATION OF AN OUTLET NOZZLE IN THE BOOSTER TANK.

DEC. 77    744      631          522         744        522
AVAILABILITY = 65X
RELIABILITY = 83X
OPEHABILITY = 82X
UTILIZATION = 7U
       THE SCRUBBER WAS OFF-LINE FOR APPROXIMATELY 109 HOURS DUE TO HIGH TRAY DIFFERENTIAL PRESSURE
       AND SOME PLUGGING IN THE I.D. FAN SENSING LINE.  THE BOILER WAS DOWN ABOUT 113 HRS. IN  DEC.

JAN. 78    744      616          416         744        416
AVAILABILITY = 5&x
RELIABILITY = 69X
OPERABILITY = 68X
UTILIZATION = 56X
       THE MODULE WAS UNAVAILABLE APPROXIMATELY 328.15 HOURS DURING JANUARY.  TWO OUTAGES WERE CAUS-
       ED BY HIGH TRAY DIFFERENTIAL PRESSURE.  AN ELECTRICAL PROBLEM BECAUSE 1A FORCED  DRAFT FAN WAS
       OUT AND LOST AIR TO THE I.D. FAN DAMPER CAUSED SOME OUTAGE TIME.  THE BOILER WAS OUT  OF
       SERVICE APPROXIMATELY 96 HRS.
                                                  92

-------
                  TABLE 3
PERFORMANCE DESCRIPTION FOR OPERATIONAL  FGO  SYSTEMS  THROUGH   01/78
 UTILITY NAME

 UNIT NAME

 UNIT LOCATION

 UNIT RATING

 FUEL CHARACTERISTICS

 FGO VENDOR

 PROCESS

 NEW OR RETROFIT

 START UP DATE

 FGO STATUS

 EFFICIENCY,
   PARTICULATE3
 NEVADA  POWER

 REIO  GARDNER  NO £

 MOAPA NEVADA

  125  MW

 COAL  0.5 - 1.0 PERCENT SULFUR

 AOL/COMBUSTION EQUIP ASSOCIATE

 SODIUM CARBONATE SCRUBBING

 RETROFIT

  4/74

 OPERATIONAL


 99 PERCENT
   S02
 85 PERCENT
  WATER  MAKE  UP
 OPEN LOOP 0.40 GPM/MW
  SLUDGE  DISPOSAL
                        SOLAR  EVAPORATION POND
  UNIT  COST
SEE APPENDIX A, KGD SYSTEM ECONOMICS
  OPERATIONAL
   EXPERIENCE
 REFER TO THE BACKGROUND INFORMATION SECTION IN TABLE 3 OF THIS REPORT.
 THIS SODIUM CARBONATE-BASED (TRONA) SCRUBBING SYSTEM CONSISTS OF ONE
 MODULE CONTAINING A TWIN VARIABLE-THROAT VENTURI SCRUBBER FOLLOWED BY  A
 SEPARATOR IN SERIES WITH A SINGLE-STAGE PERFORATED-PLATE ABSORBER TUWEK.
 PRIMARY PARTICULATE CONTROL IS PROVIDED BY UPSTREAM MECHANICAL COLLECTORS.
 A STEAM INDIRECT HOT AIR REHEAT SYSTEM RAISES THE GAS TEMPERATURE 30 F
 PRIOR TO DISCHARGE TO THE MAIN STACK. THE FLUE GAS CLEANING WASTES ARE
 ULTIMATELY DISPOSED IN AN ON-SITE CLAY-LINEO SOLAR EVAPORATION POND.
                                                93

-------
                                       BACKGROUND INFORMATION
                                                 ON
                                  REID GARDNER UNITS 1, 2, AND 3

     THE REID GARDNER POKER STATION IS LOCATED NEAR MOAPA, NEVADA, ABOUT 50 MILES NORTH  OF  LAS  VEGAS
THE STATION HAS THREE ELECTRIC POWER GENERATING UNITS,  (REIO GARDNER 1, 2, AND 3) EACH RATED  AT
125 MM.  UNITS 1 AND 2 ARE RETROFITTED WITH SODIUM CARBONATE-BASED FGD SYSTEMS.  UNIT NO. 3 IS  A  NEW
INSTALLATION, ALSO EQUIPPED WITH A SODIUM CARBONATE-BASED FGD SYSTEM.  THE COAL BURNED AT THE PLANT
HAS AN AVERAGE GROSS HEATING VALUE OF 12,a50 BTU/LB.  AND ASH AND SULFUR CONTENTS OF d AND  0.5
PERCENT RESPECTIVELY.

     THE FGD SYSTEMS INSTALLED ON REID GARDNER UNITS 1,2,43 WERE DESIGNED AND INSTALLED  BY  COM-
BUSTION EQUIPMENT ASSOCIATES IN ASSOCIATION WITH A. D.  LITTLE.  THE SYSTEMS FOR UNITS 1  AND 2 MERE
PLACED IN SERVICE IN APRIL 1974.  THE SYSTEM FOR UNIT 3 WAS PLACED IN OPERATION ON JULY  12, 1976.
THE SCRUBBING SYSTEM DESIGN WAS BASED ON INFORMATION AND DATA OBTAINED FROM AN 8000-ACFM PILOT PLANT
PROGRAM CONDUCTED AT THIS STATION IN 1971 AND 1972.

     THE FGD SYSTEM CONSISTS OF A SINGLE MODULE, DESIGNED TO HANDLE «73,000 ACFM OF GAS  AT  350 F.
THE MOOULt IS MADE UP OF A TWIN VARIABLE-THROAT VENTUHI SCRUBBER, FOLLOWED BY A SINGLE-STAGE TRAY
TOWER ABSORBER.  GAS BYPASS IS ACHIEVED BY A GUILLOTINE-TYPE DAMPER.  A COMMON FACILITY  FOR TRONA
(SODIUM CARBONATE ORE) STORAGE AND SAND REMOVAL SERVES  ALL THE FGO MODULES AT THE REID GARDNER
PLANT.  SULFUR DIOXIDE REMOVAL EFFICIENCY IS REPORTED TO BE 8b PERCENT.  PRIMARY PARTICULATE REMOVAL
IS ACCOMPLISHED BY 75 PERCENT EFFICIENT MECHANICAL COLLECTORS INSTALLED UPSTREAM OF THE  WET SCRU-
BBERS.  THE TOTAL PARTICULATE REMOVAL EFFICIENCY OF THE MECHANICAL COLLECTION AND WET SCRUBBING
SYSTEM EXCEEDS THE 99 PERCENT LEVEL.

     IN THIS SODIUM CARBONATE PROCESS, HOT FLUE GAS FROM THE BOILER PASSES FIRST THROUGH THE MECHAN-
ICAL COLLECTORS WHERE PRIMARY PARTICULATE REMOVAL TAKES PLACE.  PRESSURE IS THEN BOOSTED BY AN IND-
UCED DRAFT FAN BEFORE THE GAS STREAM SPLITS AS IT ENTERS THE TWIN-THROAT VENTURI SCRUBBER.  THE HOT
FLUE GAS IS QUENCHED BY A SHOWER OF CIRCULATED SODIUM-BASE LIQUOR.  THE GAS THEN ENTERS  THE TRAY
TOWER AND BUBBLES THROUGH THE RADIAL-VAiME MIST tLIMINATOR, WHERE THE REMAINING LIQUID DROPLETS CARR-
IED OVER WITH THE GAS ARE TRAPPED AND REMOVED.

     EFFLUENT FROM THE FGD SYSTEM IS FROM TwO SOURCES*   THE SLIP STREAM OF SPENT LIUUOR DISCHARGED
FROM THE RECIRCULATION TANK, AND THt ALKALINE CLARIFIER UNDERFLOW, WHICH SERVtS TO NEUTRALIZE THE PH
OF THE COMBINED LIQUOR BEFORE IT IS DISCHARGED TO THE SLUDGE SETTLING PONDS.   THE SPENT LIQUOR IS
PUMPED INTO ONE OF TWO SETTLING PONDS.  THE OVERFLOW FROM THIS POND is PUMPED TO A LARGER IS-ACRE
POND, WHERE THE BRINE IS EVAPORATED.  THE FGD SYSTEM OPERATES ON AN OPEN WATER LOOP WITH NO LIQUOR
RECYCLED TO THE MODULES FHOM THE PONDS.

     ADDITIONAL INFORMATION CONCERNING THE PERFORMANCE  OF THt SCRUBBERS INSTALLED AT THE REID
GARDNER STATIUN, INCLUDING PROBLEMS, SOLUTIONS, AND MODIFICATIONS, ARE PRESENTED IN THE FOLLOWING
TABLES.  IN ADDITION, A GENERAL PROCESS FLOW DIAGRAM OF THE SODIUM CARBONATE  SCRUBBING SYSTEM IS
PRESENTED IN APPENDIX B.
                                                 94

-------
NEVADA POWER                                                          REIQ 6ARONEH UNIT N0> £

                                             HR.
                 BOILER         MODULE       CALLED
        TOTAL  OPERATION   AVAILABLE        UPON TO  OPERATION
PERIOD    CHR.)    (HR.)         (HR.)      OPERATE       INK.)
FEB. 75
MAR. 75
APR. 75
MAY  75
JUN. 75
      DURING FEBRUARY  THE  FGD  SYSTEM  OPERATED WITH 90 PERCENT OPERABILITY ON TKONA SUPPLEMENTED
      WITH SODA ASH.   PROBLEMS INCLUDED A PLUGGED RECYCLE LINfc STRAINER, SEAL KATtR FILTERS, AND
      BOILER CONTROLS.   UNIT WAS  RESTARTED AFTER SHUTDOWN FOR 5-YEAK TURBINE OVERHAUL.  SECOND
      PERt-ORMANCE  TEST  WAS PASSED.   PROBLEMS INCLUDED ABRASION UF RUBBER-LINED PIPES AND ROUTINE
      MECHANICAL AND  INSTRUMENTAL PROBLEMS.  HIGH ASH CONTENT, UP TO dO PERCENT, HAD NO EFFECT ON
      EMISSIONS.

JUL. 75
      THE FGD  SYSTEM  OPERABILITY  FOR  THE MONTH OF JULY WAS 85 PERCENT.
AUG. 75
SEP. 75     720       645                                49fa
OPERABILITY =  77%
UTILIZATION =  69%
      THREE FORCED SCRUBBER OUTAGES  OCCURRED BECAUSE OF STRAINER PLUGGING, BROKEN BUCKET ELEVATOR,
      WORN RECIRCULATION PIPING,  AND  RUBBER LINER LEAKAGE.

OCT.  75     744       531                                464
OPERABILITY =  87%
UTILIZATION =  62X
      THREE FORCED SCRUBBER OUTAGES  WERE REPORTED FOR THE MONTH OF OCTOBER BECAUSE OF PUMP REPAIR,
      INSTRUMEN] PLUGGING, AND REPAIR OF SYSTEM PIPING LEAKAGE.

NOV.  75    720       603                                596
OPERABILITY =  99%
UTILIZATION =  63%
      THE UTILITY  PREFERS Tu REPORT  SYSTEM PERFORMANCE IN TERMS OF THE  OPERABILITY INDEX BECAUSE UF
      EASE OF  CALCULATION, REQUIRES  NU JUDGEMENT, AND REFLECTS THE ACTUAL PERFORMANCE OF 1 HE FGD
      SYSTEM  ACCURATELY IF THE REASONS FOR DOWNTIME ARE KNOWN.

DEC.  75
JAN.  76       744       691      b35           691        458
AVAILABILITY  = 72%
RELIABILITY =  66%
OPERABILITY =  66%
UTILIZATION =  62%
      BOILER  WAS  OUT  OF SERVICE A TOTAL UF 3 DAYS DURING THE MONTH.  SCRUBBER OUTAGES WERE CAUSED
      BY  FROZEN  CARBONATE LINES,  PLUGGED PRESSURE -SENSING LINES, DUCT  PRESSURE TRIPS, AND OVERHAUL
      OF  A  TRAY  RECYCLE PUMP.

FEB.  76     696       675      582            675        578
 AVAILABILITY  = 84%
RELIABILITY  =  86X
OPERAblLITY =  86%
UTILIZATION =  83%
       THE UTILITY  REPORTED FOUR SCRUBBER INACTIVE PERIODS DURING THE MONTH, THREE OF WHICH WERE
       SCRUBBER-RELATED OUTAGES.  THE FORCED SCRUBBER OUTAGES OCCURRED BECAUSE UF PLUGGING IN A
       VENTURI  PUMP, DEPLETION  OF  CHEMICAL, CHEMICAL LINE PLUGGING AND SEAL HATER PROBLEMS.

MAR.  76     744       660     495              633       395
AVAILIBILITY  = 67X
RELIABILITY =  62X
OPERABILITY =  60X
UTILIZATION a  53%
      TWO FORCED  SCRUBBER OUTAGES WERE REPORTED FOR THE MUNTH BECAUSE UF AN ELECTRICAL FAILURE AND
      PLUGGING IN  THE TRAY SYSTEM RESULTING IN A SUBSEQUENT OVERHAUL DF THE TRAY CYCLE PUMPS.

APR.  76     720       629      622            584        488
AVAILABILITY  = 85X
RELIABILITY =  83%
OPERABILITY s  77X
UTILIZATION =  68%
      FOUR FORCED  SCRUBBER OUTAGES WERE REPORTED BY THE UTILITY FOR APRIL.  PROBLEMS ENCOUNTERED
      WERE;   PLUGGED  SENSING LINES,  A REHEATER LEAK, VENTURI SPOOL RECYCLE REPLACEMENT, AND  TANK
      PATCHING.
                                                   95

-------
NEVADA POWER                                                      REI°  GARDNER  UNIT NO. 2

                                             HR.
                  BOILER       MODULE      CALLED
           TOTAL OPERATION   AVAILABLE     UPON TO   OPERATION
PERIOD     (HR.)   (Hk.)       (HR.J                    (HR.)

MAr  76
AVAILABILITY = 99%
RELIABILITY = 98%
OPERABlLlTY = 83%
UTILIZATION 3 79%
      PROBLEMS ENCOUNTERED DURING THE MONTH  INCLUDED PLUGGED VEMTURI LINES  AND  A  PLUGGED SENSING
      LINE.  TOTAL SCRUBBER OPERATION TIME TO DATE IS 9,488 HOURS.

JUL. 76     744     518      676              43        421
AVAILABILITY = 9ix
RELIABILITY = 96%
OPERAblLITY = 81*
UTILIZATION = b7X
      TWO FORCED SCRUBBER OUTAGES WERE REPORTED DURING  THE MONTH.  A PROBLEM WITH  A  HIGH SOLIDS
      CONCENTRATION IN  IHE VENTURI  SCRUBBING CYCLE AND  THE REPLACEMENT  OF A RUBBER-LINED PIPE IN
      THE VENTURI SCRUBBER RESULTED IN AN OUTAGE TIME OF APPROXIMATELY  19 HOURS.

AUG. 76     744      709      710            564        530
AVAILABILITY = 95%
RELIABILITY = 94X
OPERABlLlTY = 7b%
UTILIZATION = 71%
      FORCED SCRUBBER OUTAGE TIME TOTALED 34.5 HOURS.   TWO TRIPS  OCCURRED DURING  THE  MONTH  BECAUSE
      OF LEAKAGE IN THE VENTURI RECYCLE LINt AND PLUGGING IN THE  THICKENER  TANK.   THE REMAINING
      SCRUBBER OUTAGE TIME DURING THE MONTH  RESULTED FROM DEPLETION OF  CHEMICAL ABSORBENT  (TRONA)
      AND BOILER TRIPS.

SEP. 76     720      681      677            697        653
AVAILABILITY = 94%
RELIABILITY = 94X
OPEKABILITY = 96X
UTILIZATION = 91%
      TWO FORCED SCRUBBER OUTAGES,  TOTALING  43.5 HOURS  OF OUTAGE  TIME,  WERE REPORTED  BY  THE
      UTILITY DURING THE MONTH.  MINOR TRIPS WERE CAUSED BY PLUGGING IN THE I.D. FAN  REFERENCE  LINES
      AND A FALSE HIGH  TEMPERATURE  HEADING IN THE VENTURI CAUSED  BY WATER IN THE  INSTRUMENT.

OCT. 76     744      694      708            692        656
AVAILABILITY = 95%
RELIABILITY = 95%
OPERABlLlTY = 95%
UTILIZATION = 88%
      TOTAL FORCED OUTAGE TIME FOR  THE MONTH AMOUNTED TO APPROXIMATELY  36 HOURS.   SCRUBBER  TRIPS
      WERE CAUSED BY VENTURI GAS DAMPER PROBLEMS, PLUGGING IN THE SCRUBBER EFFLUENT LINE, AND RE-
      PLACEMENT OF THE  CARBONATE FEEO LINE,  SCRUBBER OUTAGE TIME DUE TO BOILER TRIPS AMOUNTED  TO
      APPROXIMATELY 65  HOURS.

NOV. 76      730      621      374           709        363
AVAILABILITY = 52X
RELIABILITY = 51%
OPERABlLlTY = 58%
UTILIZATION = 50%
      DURING A BOILER OUTAGE TO REPAIR A CONDENSER TUBE LEAK AND  BOTTOM ASH NOZZLE, THE  SCRUBBER'S
      GUILLOTINE DAMPERS WERE BADLY DAMAGED, AND THE SCRUBBER REMAINED  OUT OF SERVICE DURING  THE
      MONTH OF DECEMBER.

DEC. 76      744      275        0             00
ALL INDEX VALUES = OX

JAN. 77      744        00             00
ALL INDEX VALUES = OX
      THE BOILER WAS OFF-LINE DURING JANUARY FOR MAINTENANCE.

FEB. 77     672      516      623            431        387
AVAILABILITY = 93%
RELIABILITY = 88%
OPERABlLlTY = 75%
UTILIZATION = 56%
      TWO MINOR SCRUBBER OUTAGES RESULTED FROM A VENTURI PIPING LEAK WASH TRAY RECYCLF  TANK
      CLEANING.  AT THE END OF  THE MONTH, THERE WERE SOME ELECTRICAL PROBLEMS
                                                  96

-------
NEVADA POWER
                                                                  REID GARDNER UNIT NO. 2

                                              HR.
                  BOILER        MODULE       CALLED
           TOTAL OPERATION    AVAILABLE      UPON TO   OPERATION
PERIOD     (HR.)    (HR.)        (HR.)        OPERATE     (HR.)

MAR. 77     744      659       688             535        s&7
AVAILABILITY a 92X
RELIABILITY a 97X
OPERABILITY a 8&X
UTILIZATION a 76X

                                                          PROBLEMS,  A PLUGGED SPRAY TRAY, DUCT
APR. 77     720      720       685             685        685
AVAILABILITY a 95X
RELIABILITY a 95X
OPERABILITY = 95X
UTILIZATION a 95X
        THE SCRUBBER MODULE  REMAINED IN SERVICE ON A CONTINUOUS BASIS THROUGHOUT THE MONTH.   THE
      SYSTEM WAS FORCED OUT  OF THE  GAS PATH ON JUNE 39 BECAUSE OF A LEAK IN THE VENTURI  DISCHARGE
      LINE  (FORCED OUTAGE  TIME a  34.67 HOURS).

MAY  77     744      524       734             455        445
AVAILABILITY = 99X
RELIABILITY = 98X
OPERABILITY = 85X
UTILIZATION = 60X
       THE  SCRUBBER MODULE WAS TAKEN OUT OF THE SAS PATH TWICE DURING MONTH.   BOILER OUTAGE  (256
       HOURS) AND ONE  FORCED SCRUBBER OUTAGE (NO EMERGENCY  SPRAY  BECAUSE THE  ASH SERVICE  PUMPS HERE
       OUT  FOR APPROXIMATELY 10 HOURS).

JUN. 77     720      634       679             636        596
AVAILABILITY = 94%
RELIABILITY = 94X
OPERABILITY = 93X
UTILIZATION = 83X
       FOUR OUTAGES WERE REPORTED.   THREE WERE FORCED SCRUBBER OUTAGES DUE  TO PLUGGING OF THE  ID
       FAN  SENSING LINE, A BREAKER  TRIP RESULTING IN LOSS OF  CONTROL POWER  AND PLUGGED SPRAY  NOZZLES
       IN THE VENTURI.  TOTAL FORCED SCRUBBER OUTAGE TIME WAS APPROXIMATELY 41 HOURS FOR  THE  MONTH.

JUL. 77      744       733       298            744        298
AVAILABILITY a 40X
RELIABILITY = 40X
OPERABILITY = 41X
UTILIZATION a 40X
       EIGHT FORCED SCRUBBER OUTAGES WERE REPORTED, SEVEN OF  WHICH WERE DUE TO A HIGH/LOW TRIP IN
       SCRUBBER DUCT.  ONE TWO HOUR OUTAGE WAS REQUIRED TO  CORRECT A PLUGGING PROBLEM IN  THE
       VENTURI SPRAY NOZZLES.

AUG. 77     744      629       590             744        590
AVAILABILITY a 87X
RELIABILITY a 87X
OPERABILITY = 91X
UTILIZATION = 79X
       A LEAK IN THE VENTURI RECYCLE HEADER AND A SCRUBBER  DUCT HI-LO BOILER  TRIP PROBLEM WERE THE
       SCRUBBER RELATED OUTAGES DURING THE MONTH OF AUGUST.  THERE ALSO WAS A BOILER OUTAGE.

SEP. 77     720      716       488             693        462
AVAILABILITY a 74X
RELIABILITY = 71X
OPERABILITY a 67X
UTILIZATION a 64X
       OUTAGES DURING  SEPTEMBER RESULTED FROM A LEAK IN THE VENTURI RECYCLE LINES,  TRAY  RECYCLE
       PUMP REPAIR AND DUCT  PRESSURE HI-LO SENSING LINE PLUGGING.  OUTAGES  ALSO OCCURRED  WHEN  THE
       ASH  SLUICE SYSTEM WENT OUT OF SERVICE (NO EMtRBENCY  SPRAYS), WHEN A  TRAY PLUGGED  AND  ONE
       OCCURRED TO ALLOW CLEANING OF A SUCTION SCREEN IN THE  TRAY RECYCLE TANK.

OCT. 77     744      704       564             742        562
AVAILABILITY = 76X
RELIABILITY a 76X
OPERABILITY a 80X
UTILIZATION s BOX
       THE SCRUBBER WAS DOWN FOR  157 HOURS IN OCTOBER.  THE SCRUBBER-RELATED  OUTAGE TIME  WAS NEEDED
       TO CLEAN A PLUGGED  TRAY RECYCLE TANK SCRtEN AND A SEPARATOR TO THE VENTURI TANK.   ALSO, A
       HIGH SOLIDS PROBLEM IN THE VENTURI RECYCLE SYSTEM HAD  TO BE CORRECTED, A SCRUBBER  DUCT HI-LO
       PRESSURE BOILER TRIP  WAS REPAIRED AND ID FAN LEAKS WERE PATCHED.
                                                  97

-------
NEVADA POWER
                                                                 REID GARDNER  UNIT  NO.  2
                  BOILER       MODULE
           TOTAL OPERATION   AVAILABLE
PERIOD     (HR.)   (HR.)       (HR.)
                      96      622
                                             HR.
                                           CALLED
                                           UPON TO
                                           OPERATE

                                              98
                                                     OPERATION
                                                        (HR.)
NOV. 77     720
AVAILABILITY ' 86X
RELIABILITY = OX
OPERABILITY « OX
UTILIZATION « OX
       THE BOILER WAS OUT OF SERVICE FROM OCTOBER 31 UNTIL NOVEMBER 26.
       SERVICE FOR AN 10 FAN ROTOR REPAIR.

                                0            7
-------
                  TABLE 3
PERFORMANCE DESCRIPTION FOR OPERATIONAL  F6D  SYSTEMS THROUGH  01/78
 UTILITY NAME

 UNIT NAME

 UNIT LOCATION

 UNIT RATING

 FUEL CHARACTERISTICS

 FGD VENDOR

 PROCESS

 NEW OR RETROFIT

 START  UP DATE

 FGD STATUS

 EFFICIENCY,
   PART1CULATES
NEVADA POWER

REID GARDNER NO 3

MOAPA NEVADA

 125 MM

COAL 0.5 - 1.0 PERCENT SULFUR

AOL/COMBUSTION EQUIP ASSOCIATE

SODIUM CARBONATE SCRUBBING

NEW

 7/76

OPERATIONAL

99 PERCENT
   S02
                        65 PERCENT
  MATER  MAKE  UP
                        OPEN LOOP 0.40 GPM/MW
  SLUDGE  DISPOSAL
SOLAR EVAPORATION  POND
  UNIT  COST
  OPERATIONAL
   EXPERIENCE
REFER  TO  THE  BACKGROUND  INFORMATION  StCTION  IN  TABLE  3  OF  THIS  REPORT.
THIS UNIT  IS  A  NEW  COAL-FIHED  BOILER  THAT  IS  EQUIPPED WITH  SODIUM
CARBONATE-BASED(TKONA)SCRUB8ING  SYSTEM  WHICH  INCORPORATES  A T«IN
VARIABLE-THROAT  VENTURI  SCRUBBER  FOLLOWED  BY  A  SEPARATOR  IN SERIES  WITH
A SINGLE-STAGE  PERFORATED-PLATE  ABSORBER  TOWER.   THE  MODULE WAS FIRST
PLACED IN  SERVICE ON  BOILER  FLUE  GAS  IN JULY  1976.  MECHANICAL  COLLECTORS
PROVIDE PRIMARY  PARTICULATE  CONTROL.  REHEAT  IS  PROVIDED  BY A  STEAM IN-
DIRECT HOT  AIH  REHEAT SYSTEM.  WASTE  DISPOSAL IS ON-S1TE  CLAY-LINED POND.
                                                99

-------
                                       BACKGROUND INFORMATION
                                                 ON
                                  REID GARDNER UNITS If 2, AN[) 3

     THE REID GARDNER POWER STATION IS LOCATED NEAR MOAPA, NEVADA, ABOUT  50  MILES  NORTH OF LAS VEGAS
THE STATION HAS THREE ELECTRIC POWER GENERATING UNITS, (REID GARDNER  1, 2, AND  3)  EACH RATED AT
125 Mw.  UNITS I ANO 2 ARE KETRUFITTED wITH SODIUM CARBONATE-BASED FGD SYSTEMS.  UNIT  NO.  3 IS A NEW
INSTALLATION, ALSO EQUIPPED WITH A SODIUM CARBONATE-BASED FGD SYSTEM.  THE COAL  BURNED AT  THE PLANT
HAS AN AVERAGE GROSS HEATING VALUE OF 12.15U BTU/LB.  AND ASH AND SULFUR  CONTENTS  OF 8 AND 0.5
PERCENT RESPECTIVELY.

     THE FGD SYSTEMS INSTALLED ON REID GARDNER UNITS 1,2,8.3 WERE DESIGNED AND INSTALLED BY COM-
BUSTION EQUIPMENT ASSOCIATES IN ASSOCIATION WITH A. D. LITTLE.  THE SYSTEMS  FOR  UNITS  I AND 2 WERE
PLACED IN SERVICE IN APRIL 197*4.  THE SYSTEM FOR UNIT 3 WAS PLACED IN OPERATION  ON  JULY 12,  1976.
THE SCRUBBING SYSTEM DESIGN WAS BAStD ON INFORMATION AND DATA OBTAINED FROM  AN 8000-ACFM PILOT PLANT
PROGRAM CONDUCTED AT THIS STATION IN 1971 AND 1972.

     THE FGD SYSTEM CONSISTS OF A SINGLE MODULE, DESIGNED TO HANDLE 173,000  ACFM OF GAS AT 350 F.
THE MODULE IS MADE UP OF A TWIN VARIABLE-THROAT VENTURI SCRUBBER, FOLLOWED BY A  SINGLE-STAGE  TRAY
TOWER ABSORBER.  GAS BYPASS IS ACHIEVED BY A GUILLOTINE-TYPE DAMPER.  A COMMON FACILITY FOR  TRONA
(SODIUM CARBONATE ORE) STORAGE AND SAND REMOVAL SERVES ALL THE FGD MODULES AT THE  REID  GARDNER
PLANT.  SULFUR DIOXIDE REMOVAL EFFICIENCY is REPORTED TO BE as PERCENT.   PRIMARY PARTICULATE  REMOVAL
IS ACCOMPLISHED BY 75 PERCENT EFFICIENT MECHANICAL COLLECTORS INSTALLED UPSTREAM OF THE WET  SCRUB-
BERS.  THE TOTAL PARTICULATE REMOVAL EFFICIENCY OF THE MECHANICAL COLLECTION AND wET SCRUBBING
SYSTEM EXCEEDS THE 99 PERCENT LEVEL.

     IN THIS SODIUM CARBONATE PROCESS, HOT FLUE GAS FROM THE BOILER PASSES FIRST THROUGH THE  MECHAN-
ICAL COLLECTORS WHERE PRIMARY PARTICULATE REMOVAL TAKES PLACE.  PRESSURE  IS  THEN BOOSTED BY  AN IN-
DUCED DRAFT FAN BEFORE THE GAS STREAM SPLITS AS IT ENTERS THE TWIN-THROAT VENTURI SCRUBBER.   THE HOT
FLUE GAS IS QUENCHED BY A SHOWER OF CIRCULATED SODIUM-BASE LIQUOR.  THE GAS  THEN ENTERS THE  TRAY
TOW£R AND BUBBLES THROUGH THE RADIAL-VANE MIST ELIMINATOR, WHERE THE REMAINING LIQUID  DROPLETS CARR-
IED OVER WITH THE GAS ARE TRAPPED AND REMOVED.

     EFFLUENT FROM THE FGO SYSTEM IS FROM TWO SOURCES*  THE SLIP STREAM OF SPENT LIQUOR DISCHARGED
FROM THE RECIRCULATION TANK, ANO THE ALKALINE CLARIFIER UNDERFLOW, WHICH SERVES TO NEUTRALIZE  THE PH
OF THE COMBINED LIQUOR BEFORE IT IS DISCHARGED TO THE SLUDGE SETTLING PONDS.   THE SPENT LIQUOR  IS
PUMPED INTO ONE OF TWO SETTLING PONDS.  THE OVERFLOW FROM THIS POND IS PUMPED TO A LARGER  45-ACRE
POND, WHERE THE BRINE IS EVAPORATED.  THE FGD SYSTEM OPERATES ON AN OPEN rtATER LOOP WITH NO LIQUOR
RECYCLEO TO THE MODULES FROM THE PONDS.

     ADDITIONAL INFORMATION CONCERNING THE PERFORMANCE OF THE SCRUBBERS INSTALLED AT THE REID
GARDNER STATION, INCLUDING PROBLEMS, SOLUTIONS, AND MODIFICATIONS, ARE PRESENTED IN THE  FOLLOWING
TABLES.  IN ADDITION, A GENERAL PROCESS FLOW DIAGRAM OF THE SODIUM CARBONATE  SCRUBBING  SYSTEM  IS
PRESENTED IN APPENDIX 8.
                                                 100

-------
NEVADA  POWER                                                          Reio 6ARUNER UNIT N0. 3

                                              HR.
                  BOILER       MODULE       CALLED
          TOTAL  OPERATION    AVAILABLE      UPON TO   OPERATION
PERIOD     (HR.)    (HR.)       IHR.)        OPERATE     (HR.)
JUL. 76    744      692           355          449        316
AVAILABILITY = 45X
RELIABILITY « 70X
OPERABILITY * 46X
UTILIZATION s 42X
       COMMERCIAL OPERATION COMMENCED  ON  JULY 12, 1976.  FOUR OUTAGES WERE REPORTED FOR THE MONTH,
       THREE OF WHICH WERE FORCED  SCRUBBER OUTAGES.  PROBLEMS WERE ENCOUNTERED WITH A BUCKET ELE-
       VATOR MALFUNCTION AND  A HIGH  SOLIDS CONCENTRATION IN THE VENTURI SCRUBBING SOLUTION CYCLE.

AUG. 76    744      744           420          647        323
AVAILABILITY = 56X
RELIABILITY * SOX
OPERABILITY * 43X
UTILIZATION = 43X
       FORCED SCRUBBER OUTAGES RESULTED FROM AN 1.0. FAN ELECTRICAL MALFUNCTION, 1.0. FAN INSULA-
       TION, THICKENER TANK PLUGGING,  REHEATER MOTOR BURNOUT ANO DESTRUCTION OF THE VENTURI FLOOR.

SEP- 76    720      679           352          682        314
AVAILABILITY = 49X
RELIABILITY = 46X
OPERABILITY « 46X
UTILIZATION s 44X
       THE SYSTEM WAS PLACED  BACK  IN  SERVICE ON SEPTEMBER 14 FOLLOWING EXTENSIVE REPAIRS AND MOD-
       IFICATIONS FROM THE PRECEDING  MONTH.  THREE MINOR SCRUBBER TRIPS WERE ENCOUNTERED THROUGHOUT
       THE DURATION OF THE MONTH.   PROBLEMS REPORTED AT THE UTILITY WERE tWO REHEATER FAN TRIPS AND
       A VENTURI VIBRATION TRIP.

 OCT. 76    744      548           160          743        159
 AVAILABILITY = 22X
 RELIABILITY = 21X
 DPERABILITY = 29X
 JTILIZATION s 21X
       THREE FORCED SCRUBBER  OUTAGES  WERE REPORTED FOR THE MONTH.  TRIPS OCCURRED BECAUSE OF HIGH
       SOLIDS CONTENT IN THE  VENTURI  RECYCLE SOLUTION, A SCRUBBER GAS DAMPEK MALFUNCTION, AND
       VENTURI BOX.

 10V. 76     720      264           205          727        212
 WAILA8ILITY = 28%
 IELIABILITY s 29X
 IPERABILITY a 80X
 ITILIZATION = 29X
       THE SCRUBBER SYSTEM WAS NOT IN  OPERATION THE FIRST HALF OF NOVEMBER DUE TO REPAIRS OF LEAKS
       IN  THE  VENTURI SCRUBBER BOX.   THE  SYSTEM WAS RESTARTED NOV. 19, AND EXPERIENCED ONE FORCED
       OUTAGE, BECAUSE OF  A SCREW  CONVEYOR MALFUNCTION, PREVENTING CHEMICAL MIXING.

  EC. 76    744      744           737          728        721
  VARABILITY = 99X
  ELIABILITY =  99X
  PERA8ILITY =  97X
  TILIZATION =  97X
       DURING  THE MONTH, ONE  MINOR SCRUBBER OUTAGE OCCURRED BECAUSE OF REPAIRS TO THE I.D. FAN EX-
       PANSION JOINT.

  AN. 77     744      690           731          689        676
  VAILABILITY » 98X
  ELIABILITY a 98X
  PEHABILITY = 98X
  ULIZATION « 9ix
       TWO MINOR FORCED OUTAGES  WERE  THE  RESULTS OF A PLUGGED TRAY ANO A REHEATER STEAM LEAK.

  :B. 77    672      575           543          594        422
  /AILABILITY = BIX
  PLIABILITY = 72X
  'ERA8ILITY = 74X
  TILIZATION = 63X
       A TOTAL OF 117 HRS. OF DOWNTIME  WAS THE RESULT OF THREE FORCED SCRUBBER OUTAGES CAUSED BY
       PROBLEMS WITH THE UPPER TRAY.   A FOURTH OUTAGE RESULTED FROM DOWNTIME FOR CLEANING OUT THE
       SODIUM CARBONATE LINE.
                                                  101

-------
NEVADA POWER
                                                                  REID GARDNER UNIT NO. 3
PERIOD

MAR. 77
                  BOILER
           TOTAL OPERATION
           (HR.)   (HR.)
           744
                    639
  MODULE
AVAILABLE
  (MR.)

    324
  HR.
CALLtD
UPON TO
OPERATE

  637
OPERATION
  (HR.)

   334
AVAILABILITY * 44X
RELIABILITY * 52X
OPERABILITY = SIX
UTILIZATION = 442
       THE NO. 3 MODULE EXPERIENCED TWO MAJOR FORCED OUTAGES  DURING  MARCH.
       SEPARATOR REQUIRED DOWNTIME FOR CURING AND
                                                                            THE RUBBER  LINING  IN  THE
                                                  THE'SCRUBBER FAN EXPANSION JOINT  BLEW OUT.   THREE
       MINOR OUTAGES WERE CAUSED BY A PLUGGED TRAY AND  THE 035  LIMIT  SWITCH  TRIPPING.
                     709
                                618
                                             702
                                                        600
APR. 77    720
AVAILABILITY = 86X
RELIABILITY = 85X
OPERABILITY * 65X
UTILIZATION = 83X
       THREE SCRUBBER OUTAGES WERE REPORTED, TWO WERE FORCED OUTAGES.  A HIGH TRAY DIFFERENTIAL  AND
       A PLUGGED STRAINER IN THE TRAY RECYCLE TANK RESULTED IN A FORCED OUTAGE TIME OF  APPROXIMATELY
       102 HOURS.
                     470
                                467
                                              594
                                                         124
MAY   77     744
AVAILABILITY = 63X
RELIABILITY = 21X
OPERABILITY = 2bX
UTILIZATION * 16X
       THE  MODULE WAS UNAVAILABLE DURING THE FIRST THREE WEEKS  OF  THE  MONTH  BECAUSE  OF A FORCED OUT-
       AGE  REQUIRED FOR  THE REPLACEMENT OF  THE FRP LINER IN  THE  MODULE'S  SEPARATOR  SECTION.  NO
       OPERATING DATA WAS MADE AVAILABLE BY THE UTILITY FOR  THE  MONTH.   IN  ADDITION  THE REHEA1ER FAN
       BREAKER WAS RECEIVED AND THE VENTURI DAMPER.
                      70b
                                475
                                             666
                                                        443
 JUN.  77     720
 AVAILABILITY  = 98X
 RELIABILITY = 64X
 OPERABILITY = 63X
 UTILIZATION = 62X
      FOUR  SCRUBBER  OUTAGES WERE REPORTED, THREE OF WHICH WERE FORCED.   PROBLEMS  ENCOUNTERED INCLUDED
      A HIGH TRAY DIFFERENTIAL PRESSURE READING AND A  VENTURI RECYCLE LINE  THROTTLE VALUE.
                      744
                                542
                                              744
                                                         542
 JUL.  77     744
 AVAILABILITY  =  73x
 RELIABILITY  = 73X
 OPERABILITY  = 73%
 UTILIZATION  = 73X
       FIVE  FORCED  SCRUBBER OUTAGES WERE CAUSED BY A HIGH TKAY  DIFFERENTIAL  PRESSURE READING,  SCRUB-
       BER  FAN  VIBRATION PROBLEMS, AND REPAIRS TO THE  VENTUKI DISCHARGE  VALVE.
                     629
                                  375
                                              744
                                                         375
AUG. 77    744
AVAILABILITY = 70X
RELIABILITY = 63X
OPERABILITY = 63X
UTILIZATION = 50X
       DUE TO A LEAK IN VENTURI RECYCLE LINE THfc. UNIT WAS OFF THE LINE PART OF THE MONTH.   A FALSE
       ALARM DUE TO SCRUBBER OUTLET TEMPERATURE CAUSED SHUTDOWN FOR ABOUT A DAY.  BOILER WAS OUT OF
       SERVICE FOR ABOUT A WEEK DURING THIS REPORT PERIOD.

SEP. 77    720      720          736         654        646
AVAILABILITY = 90X
RELIABILITY = 99%
OPERAblLITY = 90X
UTILIZATION = 90X
       HIGH SOLIDS IN THE VENTURI RECYCLE SYSTEM CAUSED SOME TIME OFF IN SEPTEMBER.
       AND POST NEUTRALIZATION LINES WERE INSTALLED.
                                                                                      NEW EFFLUENT
 OCT.  77     744      506           171          460         455
 AVAILABILITY = 99X
 RELIABILITY = 99X
 OPERABILITY = 90X
 UTILIZATION = 61X
       THE  SCRUBBER WAS DOWN 284.42 HOURS DURING OCTOBER  FOR  A  SCHEDULED  BOILER OUTAGE.  4 45 HOURS
       ADDITIONAL OUTAGE TIME OCCURRED AS A RESULT  OF  HIGH VIBRATION  PROBLEMS ON A SCRUBBER FAN.
                                                  102

-------
IEVADA  POWER                                                       KEIO 6AROf
-------
                  TABLE 3
PERFORMANCE DESCRIPTION FOR OPERATIONAL FGD SYSTEMS  THROUGH   01/78
 UTILITY NAME

 UNIT NAME

 UNIT LOCATION

 UMIT RATING

 FUEL CHARACTERISTICS

 FGD VENDOR

 PROCESS

 NEW OR RETROFIT

 START UP DATE

 FGD STATUS

 EFFICIENCY,
  PAKTICULATES
NORTHERN INDIANA PUS SERVICE

D.H. MITCHELL NO.11

GARY INDIANA

 115 MW

COAL i.2-3.5 PERCENT SULFUR

DAVY POHERGAS/ALL1ED CHEMICAL

HELLMAN LORD/ALLIED CHEMICAL

RETROFIT

 b/77

OPERATIONAL


99.5 PERCENT
  SOI
                       90 PERCENT GUARANTEE
 WATER MAKE UP
                       CLOSED LOOP
 SLUDGE DISPOSAL
ELEMENTAL SULFUR PRODUCT
 UNIT COST
                      SEE APPENDIX A, FGO SYSTEM ECONOMICS
  OPERATIONAL
   EXPERIENCE
REFER TO THE BACKGROUND INFORMATION SECTION IN TABLE 3 OF THIS REPORT.
THIS FGD SYSTEM IS AN INTEGRATION OF THE WELLMAN-LORD SOi RECOVERY PROCES
OFFERED BY DAVY POWERGAS AND THE SOS TO SULFUR REDUCTION PROCESS DE-
VELOPED BY ALLIED CHEMICAL. DAVY POWERGAS IS THE DESIGN AND CONSTRUCTION
FIRM AND ALLIED CHEMICAL IS SYSTEM OPERATOR AND PRODUCT MARKETER.
PERFORMANCE TESTS WERE SUCCESSFULLY CUMPLETEO ON SEPTEMBER 1«, 1977. A
DEMONSTRATION YEAR COMMENCED ON SEPTEMBER 16, 1977.
                                               104

-------
                                       BACKGROUND  INFORMATION
                                                 ON
                                        O.H. MITCHELL  NO.  11
     IN  JUNE  OF  1972 THE NORTHERN INDIANA PUBLIC SERVICE CO.  (NIPSCO)  AND  THE  U.S.  ENVIRONMENTAL
PROTECTION  AGENCY  ENTERED INTO A COST-SHARED CONTRACT  FOR  THE  CONSTRUCTION AND OPERATION  OF  A
WELLMAN-LORD/ALLIED CHEMICAL FGO DEMONSTRATION PLANT.   THE  SYSTEM  WAS  INSTALLED
ON GENERATING UNIT NO. 11 AT NIPSCO'S D.H. MITCHELL  POWER  STATION  IN  GARY, INDIANA,  ON  THE  SOUTHERN
TIP OF  LAKE MICHIGAN.  UNIT NO. 11 IS RATED AT 115 MW  AND  FIRES  MIDWEST  COAL  WITH  A  HEAT  VALUE  OF
11,000  BTU/LB. AND SULFUR AND ASH CONTENTS OF 3.5  AND  10.OX  RESPECTIVELY.

     THIS UNIT WILL BE THE FIRST REGENERABLE FGD SYSTEM TO  CONTROL THE TOTAL  FLUE  GAS EMISSION  FROM
A FULL  SCALE COAL-FIRED GENERATING UNIT.  IT IS ALSO THE FIHST SYSTEM  TO RECOVER  ELEMENTAL  SULFUR
OF A MARKETABLE  QUALITY FROM THE FLUE GAS OF AN ELECTRIC UTILITY.   THE PRIMARY ENGINEERING  AND  CONS-
TRUCTION FIRM IS DAVY POWER6AS.  ALLIED CHEMICAL,  UNDER CONTRACT TO NIPSCO,  OPERATES THE  FGD FAC-
ILITY AND MARKETS THE USEFUL PRODUCTS.

     THE FGD SYSTEM CONSISTS OF THREE MAJOR PROCESS  UNITS:  A  rtELLMAN-LORO  SOS  RECOVERY  UNIT, A  DAVY
POWERGAS PURGE TREATMENT UNIT, AND AN ALLIED CHEMICAL  S02  REDUCTION UNIT.

     THE S02 RECOVERY SYSTEM INCLUDES A FLUE GAS BOOSTER BLOWER, A PRESCMU8BER (OKIFICE CONTACTOR),
A  THREE-STAGE TRAY TOWER ABSORBER, AND AN EVAPOKATOR/CRYSTALLIZER.  THE  PRESCKUBBER  is  A  VARIABLE-
THROAT VENTURI USED TO SATURATE THE FLUE GAS AND REMOVE ANY  FLYASH NOT COLLECTED  IN  THE ESP  UNIT.
THE FLYASH SLURRY is SPENT CONTINUOUSLY TO THE ASH PONDS.   THE ABSORBER  is A  THREE-STAGE  KOCH VALUE
TRAY ABSORPTION TOWER FOLLOWED BY A MIST ELIMAINTOR  AND A  STACK  GAS REHEAtER.   THE  SPENT  SCRUBBING
 (SODIUM SULFITE-BISULFITE) SOLUTION IS REGENERATED IN  AN EVAPORATOR/CKYSTALLIZEW.   HEUE THE  SOLUTION
IS HEATED UNTIL THE BISULFITE DECOMPOSES, EMITTING S02 GAS  AND PRECIPITATING  SOlHUM  SULFITE
CRYSTALS.  THESE ARE REMOVED AND REDISSOLVED IN THE  CONDENSATE FROM THE  EVAPORATOR  FOR  RECYCLE  TO
THE ABSORBER.

     A SMALL SIDESTREAM  IS REMOVED FROM THE SCRUBBING  LIQUOR  LEAVING  THE ABSORBER  AND SENT  TO THE
PURGE TREATMENT UNIT TO  REMOVE SODIUM SULFATE.  THIS SYSTEM  CONSISTS  OF  FOUR  CHILLED-WALL CRYSTALL-
 IZERS WHERE  SODIUM SULFATE CRYSTALS FORM, FOLLOWED BY  A CENTRIFUGE AND CRYSTAL UHYER.

     THE SULFUR DIOXIDE  FROM THE EVAPORATOR/Ch Y5TALLUER IS  COMPRESSED AND SENT TO  THE  ALLIED CHEM-
 ICAL 802 REDUCTION PLANTr WHERE IT IS REACTED WITH NATURAL  GAS.   THE  RESULTING ELEMENTAL  SULFUR  IS
 CONDENSED  AND STORED  IN  MOLTEN FORM, WHILE THE OFF-GASES ARE  BURNED IN A TAIL  GAS  INCINERATOR AND
 RETURNED TO  THE AbSORBER INLET.  THE ALLIED PLANT  IS DESIGNED  TO GENERATE  25  TON/DAY OF SULFUR.
     A SUMMARY OF THE PERFORMANCE OF THE WELLMAN-LORD  FGD  DEMONSTRATION  UNIT,  PROBLEMS/SOLUTIONS
 AND  MODIFICATIONS IS PROVIDED  IN THE PERFORMANCE HISTORY TABLE THAT FOLLOWS.   A SIMPLIFIED  PROCESS
 FLOW DIAGRAM  IS PROVIDED IN  APPENDIX B OF THIS REPORT.
                                                  105

-------
NORTHERN INDIANA PUBLIC SERVICE
                                                                        0.  H.  MITCHELL UNIT NO. 11
                               NIPSCO WELLMAN-LORD S02 KECOVERY SYSTEM
                                         OPERATING HISTORY
•INITIAL OPERATING EXPERIENCE*

     FOLLOWING COMPLETION OF CONSTRUCTION IN MID-1976, START-UP OF THE  VARIOUS  SUBSYSTEMS AND COM-
PONENT PARTS WAS INITIATED. DURING THE PERIOD JULY THROUGH NOVEMBER,  THREE  SUSTAINED  HUNS OF THE S02
ABSORBER AND REGENERATION SYSTEM UNDER NORMAL OPERATING CONDITIONS WERE ACHIEVED.   302  REMOVAL
EFFICIENCY WAS EQUAL TO OR GREATER THAN THE SOX PERFORMANCE CRITERIA.   UNIT  11  BOILER OPERATED 121
FULL DAYS AND 10 PARTIAL DAYS.  THE WELLMAN-LORD  S02 RECOVERY UNIT OPERATED  71  FULL  DAYS AND 23
PARTIAL DAYS.  DURING THIS PERIOD, NUMEROUS MODIFICATIONS AND CORRECTIONS TO  THE SYSTEM WERE COM-
PLETED.  THESE INCLUDED MODIFYING THE ABSORBER KOCH VALVE THAYS TO IMPROVE  TURN-DOWN,  RUBBER LINING
THE BOTTOM ABSORBER COLLECTOR TRAY, RELOCATING ANO IMPROVING TEMPERATURE CONTROL OF THE LOW
PRESSURE STEAM SUPPLY, INSTALLING IMPROVED S02 SAMPLE PROBES ANU SEVERAL REPLACEMENTS ANO MODIFI-
CATIONS TO THE PURGE SALT RECOVERY AREA.  FULLY INTEGRATED OPERATIONS INCLUDING  S02 REDUCTION AND
SULFUR RECOVERY OCCURRED IN NOVEMBER, 1976.  JANUARY THROUGH MAY 1977 - UNIT  11  BUILEK  WAS OUT-OF-
SERVICE FUR ABOUT FIVE MONTHS FOLLOWING A BOILER RELATED MISHAP WHICH OCCURRED  ON  JANUARY 15,  1977,
DURING START-UP AFTER A SCHEDULED MAINTENANCE TURN AROUND.

     ON JUNE 13, 1977 FGD OPERATIONS RESUMED FOLLOWING RETURN TO FULL SERVICE OF UNIT  11  BOILER.   BY
JUNE 15 FULLY INTEGRATED OPERATION OF THE ENTIRE FGD PLANT WAS ACHIEVED.  THROUGH  JUNE  AND JULY,
SEVERAL HUNDRED HOURS OF TOTAL SYSTEM OPERATION AT BOTH PARTIAL AND FULL LOAD WERE ACCRUED.
PERFORMANCE TESTS

     AUGUST-SEPTEMBER 1977 - PERFORMANCE TESTS COMMENCED ON AUGUST 29,  1977 ANO WERE  SUCCESSFULLY
COMPLETED ON SEPTEMBER 14, 1977.  THE TEST PERIOD INCLUDED 12 DAYS AT 92 MW FLUE GAS  EQUIVALENT  AND
3-1/2 DAYS AT 110 MW FLUE GAS EUUIVALENT.  DURING THIS PERIOD, 91  PERCENT OF  THE S02  WAS  REMOVED
WHILE BURNING COAL CONTAINING 3 PERCENT SULFUR AND 204 TONS OF ELEMENTAL SULFUR WERE  RECOVERED.   ALL
PERFORMANCE CRITERIA WERE MET INCLUDING 802 REMOVAL,  PARTICULATE EMMISSION, RAW MATERIAL  AND  UTILITY
CONSUMPTIONS AND RECOVERED SULFUR QUALITY.  THE FGD UNIT SHUT DOWN SEPTEMBER  19 AND REMAINED  IDLE
THROUGH MONTH END DUE TO COAL FEED PROBLEMS RESULTING FROM WET COAL ON THE UNIT 11 BOILER.
DEMONSTRATION PERIOD

     OCTOBER 1977 - A DEMONSTRATION PERIOD OF ONE YEAR BEGAN SEPTEMBER 16.  DURING OCTOBER,  THE FGD
UNIT OPERATED 132 HRS.  OPERATIONS WERE INTERRUPTED WHILE HEAT BALANCE TESTS WERE CONDUCTED  ON THE
UNIT 11 BOILER BY NIPSCO ANO TRW AND WERE INTERRUPTED FURTHER TO MAKE REPAIRS TO THE  802  REDUCTION
SECTION, THE EVAPORATOR, ANO THE UNIT 11 BOILER.
OPERATING SUMMARY (HOURS ANO VIABILITY PARAMETER DATA WILL BE INCLUDED IN THE NEXT REPORT.
                                                 106

-------
                  TABLE 3
PERFORMANCE DESCRIPTION FOR OPERATIONAL FGD  SYSTEMS  THROUGH   01/76
 UTILITY NAME


 UNIT NAME


 UNIT LOCATION


 UNIT RATING


 FUEL CHARACTERISTICS


 FGO VENDOR


 PROCESS


 NEW OR RETROFIT


 START UP DATE


 FGD STATUS


 EFFICIENCY,
  PARTICULATES
NORTHERN STATES POWER CO.


SHER8URNE COUNTY STATION NQ.l


BECKEK MINNESOTA


 710 MW


COAL O.a PERCENT SULFUR


COMBUSTION ENGINEERING


LIMESTONE SCRUBBING

NEW
OPERATIONAL
99 PERCENT
   502
                         PERCENT
  WATER MAKE UP
                       OPEN LOOP  1.13  GPM/MW
  SLUDGE DISPOSAL
CLAY-LINED DISPOSAL POND
  UNIT COST
                      SEE APPENDIX  A,  FGD  SYSTEM  ECONOMICS
  OPERATIONAL
   EXPERIENCE
REFER TO  THE  BACKGROUND  INFORMATION  SECTION  IN  TABLE  ^ OF  THIS REPORT.
FULL COMMERCIAL  OPEKA1ION  OF  THE  SYSTEM  BEGAN ON  MAY  1,  1976. THE SCRUB-
BING SYSTEM FOR  THIS  UNIT  CONSISTS OF  12 MODULES.  EACH SCRUBBING MODULE
INCORPORATES  A VENTURI-ROD SECTION AND A MARBLE BED ABSOR8EK FOR PAR-
TICULATE  AND  SULFUR DIOXIDE REMOVAL. A FORCED OXIDATION  SYSTEM CONVERTS
ALL THE CALCIUM  SULFITE  TO SULFATE PRIOR TO  DISCHARGE TO A CLAY-LINED
SETTLING  POND. STACK  GAS REHEAT  IS PROVIDED  BY  IN-LINE HOT rtATER TUBES.
                                               107

-------
                                       BACKGROUND INFORMATION
                                                 UN
                                 SHERBURNE CUUNTY GENERATING PLANT

     THE SHERBURNE COUNTY GENERATING PLANT OF THE NORTHERN STATES POWER COMPANY  IS  LOCATED ON THE
MISSISSIPPI RIVER IN SHfcReuRNE COUNTY NEAR BECKER, MINNESOTA.  THIS NEW POWfcH  GENERATING PLANT CUR-
RENTLY HAS TWO COAL-FIRED UNITS IN SERVICE AND 1 WO IN THE EARLY PLANNING  STAGES.  UNIT  NO. 1  IS
RATED AT 710 MH AND FIRES MONTANA COLSTRIP COAL WITH A HEATING VALUE OF 8300 8TU/LB,  AND SULFUR,
ASH, AND MOISTURE CONTENTS OF 0.8, 9.0 ANO 25.0 PERCENT, RESPECTIVELY.  IN OROER  TO MEET MINNESOTA
POLLUTION CONTROL AGENCY PARTICULATt AND S02 EMISSION STANDARDS OF 0.96 LBS. S02  ANO  0.087 LSS. PAR-
TICULATE PER MILLION BTU HEAT INPUT TO THE BOILER, THE UNIT WAS FITTED WITH A  LIMESTONE-BASED WET
SCRUBBING SYSTEM FOR SIMULTANEOUS PARTICULATE AND S02 REMOVAL.

     THE NORTHERN STATES POWER CO., SHERBURNE NO. 1  SCRUBBER DESIGN IS BASED UPON THE RESULTS OF  A
PILOT PLAN! TEST PROGRAM CONDUCTED AT COMBUSTION ENGINEERING'S (CE) KRE1SINGER DEVELOPMENT LABOR-
ATORY AND A PROTOTYPE SCRUBBER PROGRAM CONDUCTED JOINTLY BY COMBUSTION ENGINEERING  AND  NORTHERN
STATES POWER AT THE UTILITY'S BLACK DOG STATION.  THE SCRUBBING SYSTEM IS COMPRISED OF  A FIRST  STAGE
FIXED-ROD VENTURI SCRUBBER FOR PARTICULATE REMOVAL AND A MARBLE BED ABSORBER TO COMPLETE PARTICULATE
REMOVAL AND ACHIEVE THE NECESSARY SULFUR DIOXIDE REMOVAL.  THE SCRUBBING  HAS BEEN GUARANTEED  TO
REMOVE 99 PERCENT OF THE PARTICULATE MATTER ENTERING THE SCRUBBING SYSTEM, OR  MAINTAIN  AN EMISSION
0.0<* GR/OSCF, WHICHEVER OUTLET VALUE IS GREATER.  THE SULFUR OIUXIDE DESIGN REMOVAL EFFICIENCY  IS
BASED UPON THE REMOVAL OF 50 PERCENT OF THE SULFUR IN THE FUEL (MAXIMUM FUEL SULFUR CONTENT OF  1.2
PERCENT) OR MAINTAIN AN EMISSION UF 200 PPM, WHICHEVER OUTLET VALUE IS GREATER.

     THE GENERAL SCENARIO OF THE SHERBURNE NO. 1 SCRUBBING SYSTEM CONSISTS OF  12  SCRUBBING MODULES,
11 OF WHICH ARE REQUIRED FOR FULL LOAD CAPACITY.  EACH MODULE HAS A RATED FLUE GAS  CAPACITY OF
200,000 TO 220,000 ACFM AT 13b F.  AN AGITATED REACTION TANK IS LOCATED AT THE BOTTOM OF  EACH SCRUB-
BER MODULE.  THE PURPOSE OF THE REACTION TANK IS TO ALLOW COMPLETION OF SULFUR DIOXIDE  FORMATION  TO
SULFITE, PROVIDE FORCED OXIDATION OF SULFITE TO SULFATE, AND FACILITATE PRECIPITATION OF  CALCIUM
SULFATE SOLIDS.  IN FORCED OXIDATION, AIR IS BUBBLED INTO THE REACTION TANK, OXIDIZING  SULFITE  TO
SULFATE.  THE SULFATE FORMED is PRECIPITATED IN THE  REACTION TANK BY ADDITION  OF  GYPSUM  SEED
CRYSTALS.  A BLEED LINE PROVIDES THE NECESSARY SOLIDS REMOVAL TO A 160-FOOT DIAMETER CLARIFIER.
HERE THE WASTE SOLIDS (FLY ASH, CALCIUM CARBONATE, AND CALCIUM SULFATE) SETTLE OUT  AND  THE CLARIFIED
WATER IS RETURNED TO THE PROCESS.

     THE SCRUBBER MODULES ARE 2b FT X 18 FT X 60 FT  HIGH AND HAVE « IN. DEEP,  13/16 IN.  OIA.  GLASS
MARBLE PACKING IN THE MARBLE BED SECTION.  THE LIQUID FLOW RATE IN 5600 GPM PER MODULE  AND OF  WHICH
ABOUT 3500 6PM IS RECYCLED.  THE SOLIDS CONTENT OF THE SLURRY IS 8-10X BY WEIGHT  ANO THE  PH MAIN-
TAINED IS 5-5.5.  THE I.D. FANS HAVE A POWER RATING  OF 6000 HP AND THE PRESSURE DROP ACROSS EACH
MODULE IS 20 IN. WG.

     THE CLEANED FLUE GAS THEN PASSES THROUGH A DOUBLE ROW, TWO-PASS CHEVRON MIST ELIMINATOR.   RE-
HEAT OF tO F IS ADDED TO THE GAS STREAM TO PROVIDE PROTECTION TO THE DOWNSTREAM DUCTWORK,  I.D.  FAN,
AND PLUME CONTROL BEFORE FINAL DISCHARGE TO THE ATMOSPHERE.  THE CLARIFIER UNDERFLOW IS  PUMPED  TO A
SETTLING POND WHICH IS 45-FEET DEEP AND 62 ACRES IN  AREA, WITH AN 18-INCH CLAY LINING.   THE WATER IS
RECYCLED FROM THE POND BACK TO THE PROCESS.  A GENERAL FLOW DIAGRAM OF THE SHERBUHNE SCRU88ER
ARRANGEMENT IS PROVIDED IN APPENDIX B.

     INITIAL OPERATION OF THE SYSTEM COMMENCED MARCH 16, 1976.  FULL COMMERCIAL OPERATION  COMMENCED
MAY 1, 1976.  PROBLEMS ENCOUNTERED DURING INITIAL STARTUP OPERATIONS HAVE INCLUDED  THE  USUAL  MECH-
ANICAL PROBLEMS ASSOCIATED WITH A NEW SYSTEM AND SOME PLUGGING IN THE SCRUBBER INTERVALS.   SPECIF-
ICALLY, PROBLEMS HAVE BEEN ENCOUNTERED IN THE SPRAY  SYSTEM, REQUIRING THE DESIGN  OF THE  NOZZLES TO
BE CHANGED FROM PLASTIC ANO RUBBER COMPONENTS TO CERAMIC SPINNER-VANE COMPONENTS.   ALSO,  SOME PLUG-
GING PROBLEMS HAVE BEEN ENCOUNTERED IN THE SPRAY HEADERS, PRIMARY CONTACTOR, AND  MARBLE  BED.   THIS
HAS STEMMED LARGELY FROM THE MALFUNCTION OF THE STRAINER SYSTEM BECAUSE OF POOR NOZZLE  CONFIGUR-
ATIONS.  NSP IS CURRENTLY MAKING MODIFICATIONS IN THIS AREA.
                                                  108

-------
NORTHERN  STATES POWER CO.

              BOILER OPERATION TIME  AND  MODULE  OPERABILITY U)

               101  102   103  104   105   106   107   106  109  110  111  112
                                                                  SHERBURNE COUNTY STATION UNIT NO. 1
       BOILER
PERIOD    HR.
MAR.  76
APR. 76
         A PRELIMINARY SYSTEM CHECKOUT  WAS  SUCCtSFULLY COMPLETED BY PASSING AIR AND WATER THROUGH
         THE SYSTEM. FIRST COMMERCIAL OPERATION COMMENCED MAY 1, 1976. THIS IS AN INTERMIOIATE LOAD
         UNIT, OPERATING NEAR FULL  CAPACITY  DURING THE DAY AND 35 PERCENT CAPACITY AT NIGHT.
MAY  76  657    62   83   81   59
TOTAL SYSTEM AVAILABILITY = 86X
MEGAWATT-HOURS GENERATED  = SIB,050
                                    72
                                          SO
                                                    69
                                                         60
                                                              75
                                                                        67
 JUN. 76  688
 TOTAL SYSTEM AVAILABILITY = 84*
 MEGAWATT-HOURS GENERATED  = 372,450
         MODIFICATIONS ARE CONTINUING  ON THE SPKAY SYSTEM, SPRAY NOZZLES AND STRAINER SYSTEM.
                                     80
                           =  269,700
                           51    84    83
                                          76
                                               81
                                               71
                                                    75
                                                    84
                                                              63   91
                                                         81
                                                              76
                                                                   87
                                                                        69
                                                                        91
JUL. 76  512    80   62   71   81
TOTAL SYSTEM AVAILABILITY = 84X
MEGAWATT-HOURS GENERATED
AUG. lt>  705    46   93
TOTAL SYSTEM AVAILABILITY = 94X
MEGAWATT-HOURS GENERATED  = 421,110
         SINCE JULY 1, THE NO. 1 UNIT  HAS  BEEN  GENERATING 95-98 PERCENT OF REQUIRED MW-HOURS.  THE
         SLURRY NOZZLES AKE FREQUENTLY  PLUGGED  BY  PARTICLES ABOVE QUARTER INCH SIZE. NSP IS NOW
         PLANNING TO MODIFY THE DUPLEX  STRAINER SYSTEM TO ALLEVIATE THIS PROBLEM.  IN ADDITION,  THE
         DEPOSITION OF SOFT SOLIOS  IS  STILL  CONTINUING IN THE DEMISTERS AND REHEATERS.  HARD SCALE
         GYPSUM FURMATION ON THE VESSEL WALLS HAS  LEVELED OFF.  A CREW OF 70 PEOPLE is REQUIRED  TO
         MAINTAIN SCRUBBER OPERATIONS.  THE CLEANING  PROCEDURE CALLS FOR 3-4 MODULES TO  BE TAKEN OUT
         OF SERVICE EACH NIGHl. THUS,  EACH MODULE  IS CLEANED ONCE EVERY THkEE DAYS.
 SEP-  76  566    87   90     93    76    76
 TOTAL  SYSTEM AVAILABILITY  = 95  PERCENT
 MEGAWATT-HOURS GENERATED   => 349,470
                                           79
                                                85
                                                     79
                                                          85
                                                               80
                                                                         96
 OCT.  76  606    97    84     96    96    95   30   74   76   91   81   100   67
         TOTAL  SYSTEM OPERABILITY  HAS TO BE 100 PERCENT SINCE THE SCRUBBERS CANNOT BE BYPASSED TO
         OPERATE  THE  BOILER. NSP IS NOW IN THE PROCESS OF MODIFYING THE S1RAINEH DESIGN. THE DUPLEX
         UNITS  ARE  TO BE  REPLACED BY IN-TANK SCREENS AND SOOT BLOwEHS, BOTH LOCATED AT THE SUCTION
         SIDE OF  THE  SPRAY  WATER PUMP. CARBON STEEL FIN TUBE REHEAT BUNDLES ARE ALSO AN AREA OF
         CONCERN. MULTIPLE  FAILURES IN FOUR UNITS HAVE BEEN EXPERIENCED.
 NOV.  76   720     83    80     87    79    92  60
 TOTAL  SYSTEM  AVAILABILITY  =  93  PERCENT
 MEGAWATT-HOURS GENERATED   =  470,820
                                          97
                                                91
                                                     89
                                                     95
                                                          69   78
                                                          94
                                                               88
                                                                    73
                                                                    73
                                                                         93
 DEC.  76   722     88    84     87    80    71
 TOTAL SYSTEM  AVAILABILITY  =  95  PERCENT
 MEGAWATT-HOURS GENERATED   -  460,920
          THE  MODIFICATIONS OF  THE  DUPLEX STRAINER SYSTEM IS ONGOING, CURRENTLY APPROXIMATELY ONE-
          THIRD COMPLETED ON THE  UNIT MO. 1. THE UTILITY IS NOW CONDUCTING A FULL-LOAD EVALUATION
          STUDY,  ANALYZING  SYSTEM OPERATION ON 10 MODULES vs. THE DESIGNED n MODULES. THE UNIT is
          CURRENTLY  HAVING  DIFFICULTY COMPLYING WITH THE 20 PERCENT OPACITY REGULATION, DUE TO THE
          EXTREMLY FINE FLY ASH BEING £MITTED(70 PERCENT LESS THAN 1  MICRON.)
 JAN.  77   607    94    75    99    76    9fa
 TOTAL SYSTEM  AVAILABILITY  = 90  PERCENT
 MEGAWATT-HOURS  GENERATED   = 366,060

 FEB.  77   609    89    99    64    96    64
 TOTAL SYSTEM  AVAILABILITY  = 91  PERCENT
 MEGAWATT-HOURS  GENERATED   = 395,210
                                          77
                                          99
                                          95
                                                    92   81
                                               81    62
                                                         98
                                               86
                                                    93   95
                                                              40
                                                              93
                                                              83
                                                                   75   95
                                                                   98
                                                                   78
                                                                        61
 MAR.  77  743    47    92    95    93    93
 TOTAL SYSTEM AVAILABILITY  s 95  PERCENT
 MEGAWATT-HOURS GENERATED   = 510,650
         LOW OPERABILITIES ARE  DUE  PRIMARILY TO THE COMPLETION OF STRAINER MODIFICATIONS. THESE
         WERE PERFORMED ON ONE  MODULE AT A TIME. MODULE 101 WAS THE LAST TO UNDERGO MODIFICATIONS
         ANO WORK WAS COMPLETED KM  THE THIRD nEEK OF MARCH. Al THE PRESENT TIME, ALL MODULES ARE
         FITTED WITH  IN-TANK  STRAINERS.  THE 10 MODULES VS. 11 MODULES EVALUATION WILL BE RESUMED IN
         THE NEAR FUTURE.
                                                  109

-------
NORTHERN STATES POWER CO.
                                                                  SHERBUWNE  COUNTY STATION UNIT NO. 1
              BOILER OPERATION TIME AND MODULE OPERABILITY  (X)
       BOILER
PERIOD   HR.   101  102   103  104  105   106   107   108   109   110   111
APR. 77  718    84   65   92   95   96
TOTAL SYSTEM AVAILABILITY s 95 PERCENT
MEGAWATT-HOURS GENERATED  = 160,100
                                         62
                                         96
                                              73
                                              81
                                                   91
                                                        58
                                                    98    96
                                                             93
                                                              78
                                                                   90
                                                                   35
                                                                        88
                                                                        87
MAY  77  312    96   18   92   87   95
TOTAL SYSTEM AVAILABILITY = 92 PERCENT
MEGAWATT-HOURS GENERATED  = 195,790
         DURING THE REPORT PERIOD, THE UNIT WAS IN SERVICE ONLY  13 DAYS  DURING  THE  MONTH OF MAY
         BECAUSE OF A SCHEDULED TURBINE OVERHAUL EXTENDING FROM  MAY  14 TO  MID-JUNEC  JUNE 18 PROJ.)
JUN. 77  248    76   77   75   75   30
TOTAL SYSTEM AVAILABILITY = 92 PERCENT
MEGAWATT-HOURS GENERATED  » 127,290
                                         87
                                         94
                                              58
                                              91
                                                        61
                                                   17
                                                              80
                                                              83
                                                                   78
                                                                        83
                                                                        83
JUL. 77  736    93   66   92   90   92
TOTAL SYSTEM AVAILABILITY a 97 PERCENT
MEGAWATT-HOURS GENERATED  = 476,490
         THE UNIT CAME BACK ON LINE 6/18/77 AFTER COMPLETION OF THE  FIRST  YEAR  INSPECTION.  ONE OF
         THE HIGHEST AVAILABILITIES EVER DEMONSTRATED ON THIS  UNIT WAS  RECORDED  DURING JULY AS A
         RESULT OF THE COMPLETED CLEANOUT OVER THE OUTAGE. A SCRUBBER CLEANOUT  AND  STAINLESS STEEL
         MODIFICATIONS TOOK PLACE.
AUG. 77  640    85   89   66   55   81
TOTAL SYSTEM AVAILABILITY = 95 PERCENT
MEGAWATT-HOURS GENERATED  a 357,380
                                         90
                                         62
                                              83
                                              83
                                                   79
                                                   90
                                                        72
                                                        86
                                                             85
                                                             77
                                                                  90
                                                                  77
                                                                       66
SEP. 77  686    86   85   88   92   88
TOTAL SYSTEM AVAILABILITY = 95 PERCENT
MEGAWATT-HOURS GENERATED  * 416,430
         DURING AUGUST ONLY NORMAL MAINTENANCE WAS REQUIRED. IN SEPT., MODULE  106 SPRAY  WATER  PUMP
         WAS OVERHAULED. SOME ANGLES WERE INSTALLED ON THE PRIMARY CONTACTOR RODS TO  RESIST  EROSION.
OCT. 77  609    70   81   95   97   63
TOTAL SYSTEM AVAILABILITY = 88 PERCENT
MEGAWATT-HOURS GENERATED  = 360,850
                                         35
                                         82
                                              87
                                                   99
                                                   91
                                                        96
                                                             39   58
                                                                       96
                                                        89   89
                                                                  92   52
NOV. 77  705    77   91   42   86   79
TOTAL SYSTEM AVAILABILITY = 92 PERCENT
MEGAWATT-HOURS GENERATED  = 412,360
         OPERABILITES BELOW 50 PERCENT ARE DUE TO SPRAY WATER PUMP OVERHAULS.  TWENTY-FOUR  PUMPS  ARE
         BEING COMPLETELY OVERHAULED. STRAINER/WASHER SCREEN EROSION  HAS  BEEN  A  PROBLEM. REPAIR  AND
         REPLACEMENT HAS BEEN CONTINUALLY NECESSARY. 316 SS MATERIAL  KILL  BE USED  IN  FUTURE.  THE
         REPLACEMENT MATERIAL IS EXPECTED TO ARRIVE DEC. 12, 1977 AND  WORK  IS  EXPECTED  TO  TAKE
         THREE MONTHS.
DEC, 77  557    97   90   95   94   71
TOTAL SYSTEM AVAILABILITY =  93 PERCENT
MEGAWATT-HOURS 6ENERATED  =  325,050
                                         92
                                         84
                                              26   67
                                              92
                                                   64
                                                        96
                                                        91
                                                             98
                                                             80
                                                                  95
                                                                  88
                                                                        90
                                                                       82
JAN. 78  648    83   63   88   73   84
TOTAL SYSTEM AVAILABILITY = 92 PERCENT
MEGAWATT-HOURS GENERATED   = 374,290
         THE REPLACEMENT PROGRAM HAS BEGUN ON DtC.21.  IT  TAKES  4/6  DAYS  FOR  WORK  ON  EACH  MODULE.
         MODULE 107 HAD HIGH MAINTENANCE ALONG    WITH  fHfc STRAINERS  REPLACEMENT.
                                                  110

-------
                  TABLE 3
PERFORMANCE DESCRIPTION FOR OPERATIONAL  FGD  SYSTEMS THROUGH
                                                              01/78
 UTILITY NAME


 UNIT NAME


 UNIT LOCATION


 UNIT RATING


 FUEL CHARACTERISTICS


 FGD VENDOR


 PROCESS


 NEW OR RETROFIT


 START UP DATE


 FGD STATUS


 EFFICIENCY,
   PARTICULATES
NORTHERN STATES POWER  CO.


SHERBURNE COUNTY STATION  NO.


BECKER MINNESOTA


 710 MW


COAL 0.8 PERCENT SULFUR


COMdUSTION ENGINEERING


LIMESTONE SCRUBBING

NEW


 a/77


OPERATIONAL



99 PERCENT
                        5  PERCENT
  WATER MAKE UP
                        OPEN  LOOP  1.13 GPM/MW
  SLUDGE DISPOSAL
                        CLAY-LINEO  DISPOSAL POND
  UNIT COST
                       SEE  APPENDIX  A,  FGD SYSTEM ECONOMICS
  OPERATIONAL
   EXPERIENCE
REFER TO  THfc BACKGROUND  INFORMATION  SECTION  IN  TABLE  3  OF  THIS  REPORT.
THE SHERBURNE NO.  2  AIR  QUALITY  CONTROL  SYSTEM  is  IDENTICAL  IN  DESIGN  TO
THE SYSTEM  IN OPERATION  ON  THE NO.  1  UNIT  AT  THIS  STATION.  TWELVE  cJ-STAGE
PARTICULATE SCRUBBER  (VENTURI-ROD  SCRUBBER)  AND  SULFUR  DIOXIDE  ABSORBER
(MARBLE-BED ABSORBER)  MODULES ARE  PROVIDED FOR  FLY  ASH  AND  S02  CONTROL.
ELEVEN MODULES  ARE REQUIRED  FOR  FULL  GENERATING  CAPACITY OPERATIONS.
THE CALCIUM SULFITE  is FORCIBLY  OXIDIZED  TO  SULFATE PRIOR  TO  DISCHARGE TO
TM£ DISPOSAL POND. STACK  GAS REHEAT  PROVIDED  bY  IN-LINE HOT  WATER  TUBES.
                                               Ill

-------
                                       BACKGROUND  INFORMATION
                                                 ON
                                  SHERBURNE COUNTY GENERATING  PLANT

     THE SHERBURNE COUNTY GENERATING PLANT  (SHERCO) OF  THE NORTHERN  STATES  POWER COMPANY (NSP) IS
LOCATED ON THE MISSISSIPPI RIVER IN SHERBURNE COUNTY, BECKER,  MINNESOTA,  APPROXIMATELY «5 MILES
NORTHWEST OF MINNEAPOLIS.  THIS NEW POWER-GENERATING PLANT CURRENTLY  HAS  TWO  COAL-FIRED UNITS IN
SERVICE AND TWO IN THE tARLY DESIGN STAGES.  UNIT  NO. 2  IS RATED  AT  710 MW  AND  FIRES LOW SULFUR COL-
STRIP MONTANA COAL THAT HAS A HEATING VALUE OF 830  BTU/LB, SULFUR CONTENT  OF  0.8  PERCENT,  ASH
CONTENT OF 9.0 PERCENT, AND A MOISTURE CONTENT OF  25.0  PERCENT.   IN  ORDER TO  MEET  MINNESOTA
POLLUTION CONTROL AGENCY EMISSION CODES OF  o.96 LB SULFUR DIOXIDE AND  0.097 LB  ^ARTICULATES PER
MILLION BTU HEAT-INPUT TO THE BOILER, THE UNIT WAS FITTED WITH A  NON-REGENERABLE LIMESTuNE-BASEO WET
SCRUBBING SYSTEM.

     THE DESIGN OF THE SCRUBBER PLANT FOR SHERCO NO. 2  IS IDENTICAL  TO THAT EMPLOYED FOR THE NO.  1
UNIT NOW IN SERVICE AT THIS STATION (SEE THE PRECEDING  FILE IN THIS  REPORT  FOR  ADDITIONAL INFOR-
MATION).  THE SCRUBBER DESIGN IS BASED UPON PILOT  PLANT  AND PROTOTYPE  PLANT RESEARCH PROGRAMS CON-
DUCTED AT CUMBUSTION-ENGINEERING'S  (c-E) KREISINGER LABORATORY AND NSP'S  SLACK  oo& STATION.  THE
BLACK DOG PROTOTYPE UNII WAS OPERATED FOR FOURTEEN MONTHS FROM MARCH  1973 TO  MAY 1974.  NSP, C-E,
ANU BLACK & VEATCH WERE RESPONSIBLE FOT THE OPERATION OF THE isooo ACFM PROTOTYPE  SCRUBBER.  IHE
RESULTS OF THIS PROGRAM INDICATED THAT C-E  FIXED-ROD SCRUBBER  AND SINGLE-STAGE  MARbLE-BED ABSORBER
MODULES WOULD PROVIDE SUFFICIENT POLLUTANT  REMOVAL CAPABILITY  WITH MINIMAL  SCALING AND PLUGGING
PROBLEMS.  THE SCRUBBING SYSTEM HAS BEEN GUARANTEED TO  REMOVE  99  PERCENT  OF THE  INLET  PARTICULATE
MATTER ENTERING THE SCRUBBING PLANT OR MAINTAIN AN EMISSION OUTLET OF  O.OH  GR/SCF,  WHICHEVER VALUE
IS GREATER, AND REMOVE 50 PERCENT OF THE SULFUR IN THE  FUEL (MAXIMUM FUEL SULFUR CONTENT  OF 1.2
PERCENT) OR MAINTAIN AN EMISSION UUTLET OF  200 PP  M 302, WHICHEVER VALUE  IS CREATE*.

     THE SCRUBBER PLANT DESIGN FOR SHERCO NO. 2 CONSISTS OF 12 C-E VENTKI-ROO SCRUBBER AND  MARBLE
BED ABSORBER MODULES, 11 UF WHICH ARE REQUIRED FOR UNIT  FULL-LOAD CAPACITY.   EACH  MODULE  HAS A
MAXIMUM FLUE GAS CAPACITY OF 220,000 ACFM AT 135 F.  INCLUDED  IN  EACH  MODULE  IS  A  VENTUKI  SECTION
WITH TWO PARALLEL ROWS OF HORIZONTALLY ORIENTED RODS (PRIMARY  CONTACTOR), A SINGLE  STAGE  MARBLE-BED
(3.5 TO «.0-INCH DEEP BED OF 13/lb-INCH DIAMETER GLASS  SPHERES),  LADDER VANES FOR  GAS-FLOW  DISTRI-
BUTION, TWO-STAGE CHEVRON-TYPE DEMISTER, FINNED-TUBE HOT WATER HEAT EXCHANGER,  AND  AN  INTERNAL
REACTION TANK.  THE REACTION TANK IS LOCATED AT THE BOTTOM OF  EACH MODULE AND FACILITATES  THE
COMPLETION OF THE CHEMICAL ABSORPTION OF S02 TO CALCIUM  SULFITE.  IN ADDITION,  THE  SULFITE  SPECIES
FORMED IS FORCIBLY OXIDIZED TO SULFATE IN THE REACTION  TANK VIA AIR BUBBLING  AND AGITATION.   THE
SULFA1E SPECIES FORMED IS PRECIPITATED OUT  bY THE  ADDITION OF  A GYPSUM SEED Tu  THE  REACTION TANK
LIQUOR, OEWATERED IN A 160-FOOT DIAMETER CLARIFIER, AND  DISPOSED  OF WITH  IHE  COLLECTED PARTICULATE
MATTER IN AN ON-SITE 18-INCH CLAY-LINED SLUDGE FOND (2790 ACRE-FEET CAPACITY).   WATER  IS  RECYCLED
BACK TO THE SCRUBBER PLANT FROM THE DISPOSAL POND  FOR FURTHEK  SERVICE.

     THE ABSORPTION OF SULFUR DIOXIDE FKOM  THE FLUE GAS  STREAM RESULTS FROM THE  PRESENCE  OF  TwO
ALKALINE MATERIALS.  THE CALCIUM UXIDE IN THE FLY  ASH (APPROXIMATELY 17 PERCENT  UY  WEIGHT)  AND  THE
CALCIUM CARBONATE IN THE TAIL-END LIMESTONE ADDITIVE.

     ADDITIONAL INFORMATION OF THE OPERATION OF THIS UNIT IS PROVIDED  IN THE  PERFORMANCE  HISTORY
TABLE THAT FOLLOWS.  A SIMPLIFIED PROCESS FLOW DIAGRAM  OF THE  SHERCO SCRUBBER SYSTEM  IS  PROVIDED IN
APPENDIX B OF THIS REPORT.
                                                  112

-------
NORTHERN  STATES POWER CO.

              BOILER OPERATION TIME AND  MODULE  UPERABILITY (X)
        BOILER
PERIOD    HR.    201  £02  203  204  205   206   207   206  209  210  211  212
                                                                  SHERBURNE  COUNTY  STATION  UNIT  NO.
APR.  77   697      0    95   93   87    83
TOTAL SYSTEM  AVAILABILITY = 92 PERCENT
MEGAWATT-HOURS GENERATED  = 142,170
UNIT  CAPACITY FACTOR      = 78 PERCENT
                                          100
                                               94
                                                76
                                                     74
                                                     98
                                                          91
                                                          94
                                                               87
                                                               92
                                                                    85
                                                                    91
                                                                         86
                                                                         98
HAY   77   644     33   100   44   95   94
TOTAL SYSTEM  AVAILABILITY = 91 PERCENT
MEGAWATT-HOURS GENERATED  =  421,020
UNIT CAPACITY FACTOR      =  75 PERCENT
         FROM FULL SCALE STARTUP ON APRIL  1, THE  SYSTEM  HAS  BEEN  OPERATING VERY WELL  WITH  NO  MAJOR
         PROBLEMS ENCOUNTERED. THE UTILITY  IS MAINTAINING  A  SCHEDULE  OF  NIGHTLY CLEANING  ON  THE
         SCRUBBERS. THE CURRENT SCHtMt IS  SUCH  THAT  EACH MOOULE  IS  CLEANED AFTER 7-8  DAYS.
 JUN. 77  720    92    76
 TOTAL SYSTEM AVAILABILITY
 MEGAWATT-HOURS GENERATED
                           78   79   89
                          = 96 PERCENT
                          =  423,680
                                          74
67
     88
          88
               78
                    45
                         85
 JUL. 77  602    96    87   86    97    96    88   68   95   57   93   94   87
 TOTAL SYSTEM AVAILABILITY  =  97  PERCENT
 MEGAWATT-HOURS GENERATED   =  382,890
         MODULE 101 HAS BEEN IN  THE  SPRAY  TOWER MODE SINCE SEPT. 5,  1976. THIS DESIGN PAVED THE WAY
         FOR THE DESIGN ON SHERCO  NOS.  3  AND 4. THE CEILCOAT LINING  FAILURE IS OBSERVED ABOVE THE
         LIQUID LEVEL OF  INTERNAL  RECYCLE  TANK. BUBBLING AND CRACKING CAN BE SEEN HERE. THE LINER
         EXTENDS UP THROUGH  THE  MODULE  TO  THE REHEATEK.
 AUG.  77  67b    86     ?5    67    82    84
 TOTAL SYSTEM AVAILABILITY  = 93  PERCENT
 MEGAWATT-HOURS GENERATED   = 366,500
                                           35
                                           82
                                                     80
                                                     86
                                                          56
                                                          56
                                                               79
                                                               67
                                                                    71
                                                                    73
                                                                         33
                                                                         66
 SEP.  77  717    89     61    82    90    81
 TOTAL  SYSTEM AVAILABILITY  = 94  PERCENT
 MEGAWATT-HOURS GENERATED   = 423,280
         MOOULE 206  AND 209 SPRAY  PUMPS  WERE OVERHAULED. THE NOZZLES REQUIRED EXTENSIVE CLEANING.
         THE STRAINERS IN  MODULE 207  AND 209 REACTION TANKS HAVE STARTED ERODING. NSP ANTICIPATES
         REPLACING  THEM VERY  SOON.
 OCT.  77   b64     96     89    67    66   62
 TOTAL SYSTEM  AVAILABILITY  = 95  PERCENT
 MEGAWATT-HOURS  GENERATED   = 449,140
                                           99   98
                                           73   75
                                                     93
                                                     66
                                                          96
                                                          94
                                                               96
                                                               77
                                                                    70
                                                                         81
                                                                     91  65
 NOV.  77   715     85     93    68    80   93
 TOTAL SYSTEM  AVAILABILITY  = 91  PERCENT
 MEGAWATT-HOURS  GENERATED   = 435,360
          LOW  OPERABILITIES ARE  DUE TO SPRAY WATER PUMP OVERHAULS. 24 PUMPS ARE BEING OVERHAULED.
          STRAINER/WASHER  SCREEN EROSION HAS BEEN A PROBLEM. 316 S3 MATERIAL WILL BE USED IN FUTURE.
          REPLACEMENT  MATERIAL  IS EXPECTED TO ARRIVE DECEMBER 12, 1977 AND WORK IS EXPECTED TO LONG
          FOR  THREE  MONTHS.
 DEC.  77   733     53     93    94    81    89
 TOTAL SYSTEM  AVAILABILITY  = 93  PERCENT
 MEGAWATT-HOURS  GENERATED   = 443,500
                                           95   93
                                           67
                                                91
                                                     83
                                                     88
                                                          62   62
                                                          77
                                                               72
                                                                    90
                                                                    73
                                                                         92
                                                                         84
 JAN.  78   682     91     75    64    72   74
 TOTAL SYSTEM  AVAILABILITY  = 92  PERCENT
 MEGAWATT-HOURS  GENERATED   = 387,190
          THE  REPLACEMENT  OF STRAINER SCREENS HAS BEGUN ON DEC. 21. IT TAKES 4-6 DAYS FOR WORK ON
          EACH MOOULE.
                                                  113

-------
                  TABLE 3
PERFORMANCE DESCRIPTION FOR OPERATIONAL FGD SYSTEMS  THKOUGH
                                       01/78
 UTILITY NAME

 UNIT NAME

 UNIT LOCATION

 UNIT RATING

 FUEL CHARACTERISTICS

 FGD VENDOR

 PROCESS

 NEW OR RETROFIT

 START UP DATE

 FGD STATUS

 EFFICIENCY,
  PARTICULATES
 PENNSYLVANIA POWER CO.

 BKUCE MANSFIELD NO. 1

 SHIPPINGPORT PENNSYLVANIA

  aas MW

 COAL 4.7 PERCENT SULFUR

 CHEMICO

 LIME SCRUBBING

 NEW

  fl/76

 OPERATIONAL


 99.B PERCENT  DESIGN
  302
                       92 PERCENT  (DESIGN)
 WATER MAKE UP
                       OPEN LOOP
 SLUDGE DISPOSAL
                       RESERVOIR LANDFILL
 UNIT COST
SEE APPENDIX A, FGD SYSTEM ECONOMICS
 OPERATIONAL
  EXPERIENCE
 THIS EMISSION CONTROL SYSTEM WAS DESIGNED TO REMOVE FLYASH ANO S02 FROM
 J5.3b MM ACFM OF FLUE GAS VIA WET LIME SCRUBBING. THE INITIAL SHAKEDOWN
 AND DEBUGGING PHASE OF OPERATION BEGAN FOR PART OF THE SYSTEM IN DECEMBER
 1975. PARTIAL COMMERCIAL OPERATION COMMENCED IN APRIL 1976. THE UNIT WAS
 CERTIFIED FULL-LOAD CUMMERCIAL IN JUNE 1976. THE FGO SYSTEM HAS EXPERI-
 ENCED OPERATIONAL PROBLEMS SINCE IT HAS BEEN IN SERVICE REQUIRING A NUM-
 BER OF SYSTEM REPAIRS AND DESIGN MODIFICATIONS. REFER TO BACKGROUND IN-
 FORMATION SECTION IN TABLE 5 OF THIS REPORT FOR GREATER DETAIL.
                                               114

-------
                                       BACKGROUND  INFORMATION
                                                 ON
                                     BRUCE MANSFIELD  UNIT  NO.  1

     THE  BRUCE  MANSFIELD PLANT IS A 2475 NET MW, THREE-UNIT, COAL  FIRED  FACILITY  LOCATED  ON  THE  OHIO
RIVER IN  THE  BOROUGH OF SHIPPINGPORT, PENNSYLVANIA.   THIS  NEW  FACILTTY  IS  BEING  BUILT  BY  PENN-
SYLVANIA  POWER  COMPANY, ACTING ON ITS OWN BEHALF AND  AS  AGENT  FOR  THE  OTHER  PARTICIPATING  CENTRAL
AREA  POWER  COORDINATION (CAPCO) GROUP OF INVESTOR-OWNED  ELECTRIC UTILITIES,  INCLUDING  THE  CLEVELAND
ELECTRIC  ILLUMINATING COMPANY, OUUUESNE LIGHT COMPANY, OHIO  EDISON COMPANY,  AND  TOLEDO tOlSON
COMPANY.

     BRUCE  MANSFIELD NO. 1 IS A COAL-FIRED, ONCE-THROUGH,  SUPERCRITICAL  STEAM  GENERATOR WHICH FIRES
333 TONS/HR OF  COAL GENERATING APPROXIMATELY b.b MM LB/HR  OF STEAM AT  3,765  PSIG,  1005 F/1005 f.
THE EMISSION  CONTROL EQUIPMENT REQUIRED FOR THIS UNIT  IS DESIGNED  TO  MEET  STATE  EMISSION  REGULATIONS
OF O.t> LBS  SULFUR DIOXIuE/MM 6TU OF HEAT INPUT  AND 0.0175  GR/bCF OF PARTICULATE  WHEN BURNING  11,900
BrU/LB COAL HAVING AVERAGE ASH AND SULFUR CONTENTS UF  12.5 AND 1.7 PERCENT,  RESPECTIVELY.

     IN LATE  1970, AN INTENSIVE INVESTIGATION Of MOKE  THAN 30  POTENTIAL  OESULFURIZATION SYSTEMS  WAS
INITIATED.   THE SYSTEM ULTIMATELY CHOSEN FOR THE REMOVAL OF  FLY  ASH AND  SULFUR OIuXIDE WAS THE
VENTURI wET-SCRUBblNG SYSTEM, PROVIDED BY CHEMICO  AIR  POLLUTION  CONTROL  CO.,  UTILIZING THE DRAVO
CORPORATION'S THIOSORBIC LIME AS THE SCRUBBING  ABSORBENT.

     THE DESIGN FEATURES OF THE SCRUBBING SYSTEM DICTATE THAT  EACH SCRUBBING  TRAIN  CONSIST OF A
SCRUBBING VESSEL (VARIABLE-THROAT VENTURI), A 9000 HP  I.D. FAN,  AND AN  ABSORBER  VESSEL IF IXEO-THROAT
VENTURI).  THERE ARE SIX SCRUbBER TRAINS PER UNIT  TO  HANDLE  THE  FLUE  GAS FLOW  FROM  EACH BOILER AT
FULL LOAD (JS.iS MM ACFM AT 285 F).  THE SCRUBBER/ABSORBER  TRAINS ARE  ARRANGED  IN  TWO GROUPS OF
THREE.  THE TREATED FLUE GAS, WHICH HAS PASSED  THROUGH tACH  GROUP  OF  THE SCRUBBING  SYSTEM  TRAINS IS
DUCTED THROUGH UNE OF THE TWO HEAT CHAMBERS AND THEN  DISCHARGED  FRUM  ONE OF  TWO  CHIMNEY FLUES.   THE
950  FOOT CHIMNEY CONTAINS FOUR CARBON STEEL FLUfcS.  THE  INNER  SURFACES  OF  flHICH  ARE COATED rtlTH
POLYESTER FLAKEGLASS LINING AND ARE CAPABLE OF  ACCOMODATING  TWO  UNITS  AT FULL  LOAD.

     THE ADJUSTABLE VENTURI THROAT SCRUBBING MODULES  REMOVE  MOST OF THE  FL*ASH CONTAINED  IN THE  FLUE
GAS.  THE ABSORBER MODULE, WHICH IS A FIXED-THROAT VENTURI,  REMOVES SOME OF  ThE  REMAINING  FLYASH.
SULFUR DIOXIDE IS ABSORBED IN BOTH THE SCRUBBER AND ABSORBER BY  DROPLETS OF  LIME  SLURRY,  CONTAINING
2  TO b PEKCENT MAGNESIUM OXIDE.

     THE SCRUBBER-RECYCLE BLEED IS COMBINED WITH A FLYASH  SLURRY FROM  THE  BOILER  AND DISCHARGED  TO A
200-FOOT DIAMETER THICKENER.  SLUDGE FRUM THE THICKENER  IS THEN  PUMPED  TO  A  WASTE  DISPOSAL SYSTEM
WHERE IT IS MIXED WITH A STABILIZING AGENT  CCALCILOX)  AND  THEN PUMPED  APPRUXIMATELY 7  MILES TO THE
LITTLE BLUE RUN DISPOSAL AREA.  THE DISPOSAL AREA  IS  LOCATED IN  A  RAVINE UPSTREAM  OF A 000 FT HIGH
HYDRAULIC DAM DESIGNED TO CONTAIN THICKENER SLUDGE AND WATER.

     A SIMPLIFIED PROCESS FLOW DIAGRAM IS PRESENTED IN APPENDIX  B.
SINCE THE UNIT COMMENCED COMMERCIAL OPERATION IN APRIL 1976, A NUMBER  OF PROBLEM  AREAS HAVE BEEN
ENCOUNTERED.  MAJOR AREAS OF  CONCERN ARE SPECIFIED bELOw:
                    1.  EXCESSIVE MAINTENANCE PROBLEMS WITH  THE  WET I.D. FAN  HOUSINGS.
                    2.  EXCESSIVE WATER ENTRAINMENT AND  CARRY  OVER OUT  UF  THE  STACK CAUSING A STACK
                        RAIN  PROBLEM.
                    3.  REHEAT BURNER PROBLEMS.
                    *t.  STACK FLUE LINER FAILURES.

      ADDITIONAL  INFORMATION CONCERNING THE  PERFORMANCES  OF THIS  SYSTEM,  INCLUDING  REMOVAL  EFFIC-
 IENCY, PROBLEMS AND SOLUTIONS  ARE PROVIDED  IN THE  PERFORMANCE  TABLE THAT FOLLOWS.
                                                  115

-------
PENNSYLVANIA POWER CO.
                                                   BRUCE MANSFIELD  UNIT  NO. 1
MONTH  BOILER

DEC. 75



JAN. 76



FEB. 76
APR. 76  506
        OPERATING HOURS
          FSD MODULES                               COMMENTS
   A    B    C    D    E    F
                                INITIAL OPERATION  (SHAKEDOWN AND  DEBUGGING)  FOR PART OF
                                THt SYSTEM COMMENCED  IN DECEMBER  1975.

                                UNIT SHUT DOWN FOR ONE WEEK BECAUSE  OF  PLUGGED MIST
                                ELIMINATORS AND I.D.  FAN HOUSING  VIBRATION  PROBLEMS.


                                FIRST ATTEMPTS AT  STARTING UP  THE  REHEAT  BURNERS WERE
                                MADE THIS MONTH.   SO  MANY PROBLEMS ENCOUNTERED THAT THE
                                VENDOR IS GOING TO REDESIGN NEW REHEAT  BUHNERS.


   0* 210* 984* 2147* 2808*2427*THt INSTALLATION BEGAN PARTIAL COMMERCIAL OPERATION
                                APRIL 5.  THE SCRUBBING SYSTEM IS  CURRENTLY  HANDLING
*NOTE - THESE FIGURES REPRESENT FLUE GAS AT A TOTAL EQUIVALENT CAPACITY OF  APPROXIMATE-
                                LY 640 MW (GROSS).  TOTAL MOOULE BY  MODULE  UPERATION
                                HOURS LOGGED TO-UATE  ARE POSTED IN THE  ACCOMPANYING
                                TABLE.
                     TOTAL OPERATING HOURS
                     ACCUMULATED TO DATE.
MAY  76  595   209  605  592  492  622  493  THE LAST SCRUBBER TRAIN  WAS  PLACED  IN  SERVICE  DURING
TOTAL SYSTEM AVAILABILITY = sox
TUTAL SYSTEM OPERABILITY = IOOX
TUTAL SYSTEM RELIABILITY = IOOX
TOTAL SYSTEM UTILIZATION = 60%
JUN. 76  720   714  660  701  674
TOTAL SYSTEM AVAILABILITY = ioox
TOTAL SYSTEM OPERABILITY = IOOX
TOTAL SYSTEM RELIABILITY = ioox
TOTAL SYSTEM UTILIZATION * 10UX
JUL. 76  673   537  590  606  637
TOTAL SYSTEM AVAILABILITY = 901
TOTAL SYSTEM OPERABILITY = 100%
TOTAL SYSTEM RELIABILITY = IOOX
TOTAL SYSTEM UTILIZATION = 90X
                      705  573
                      662  661
 AUG. 76  705
 TOTAL SYSTEM
 TOTAL SYSTEM
 TUTAL SYSTEM
 TOTAL SYSTEM

 SEP. 76  720
 TOTAL SYSTEM
 TOTAL SYSTEM
 TOTAL SYSTEM
 TOTAL SYSTEM

 OCT. 76  720
 TOTAL SYSTEM
 TOTAL SYSTEM
 TOTAL SYSTEM
 TOTAL SYSTEM

 NOV. 76  277
 TUT»L SYSTEM
 TOTAL SYSTEM
 TOTAL SYSTEM
 TOTAL SYSTEM
  672  620  653  535
AVAILABILITY s 95X
OHERABILITY = IOOX
RELIABILITY = IOOX
UTILIZATION = 95X


  708  617  693  695
AVAILABILITY = IOOX
OPERABILITY = IOOX
RELIABILITY x IOOX
UTILIZATION = IOOX


  708  617  693  695
AVAILABILITY = 99X
OPERABILITY = IOOX
RELIABILITY = IOOX
UTILIZATION = 99X


  270  278  262  113
AVAILABILITY = 38X
OPERABILITY = IOOX
RELIABILITY r IOOX
UTILIZATION 3 38X
500  668
596  464
596  464
159  246
THE MONTH.  SERVICE TIME TOTALS FOR ALL 6  SCRUBBER-AB-
SORBER TRAINS THROUGH MAY ARE POSTED  IN THE  ACCOMPANY-
ING TABLE ALONG WITH THE PERFORMANCE  INDEX VALUES.
DURING OFF-PEAK HOURS ON THE WEEKENDS WHEN THE  UNIT  IS
OPERATING AT REDUCED LOADS MAINTENANCE IS  PERFORMED  ON
THE SHUT DOWN FGO MODULES SO THAT THEY WILL  BE  IN OPER-
ATING CONDITION FOR FULL LOAD OPERATION DURING  THE HIGH
DEMAND HOURS.

THE UNIT WAS DECLARED COMMERCIALLY AVAILABLE FOR FULL
LOAD OPERATION AT 825 MW (NET) ON JUNE 1,  1976.  IN-
STALLED THE REVISED SCRUBBER BAFFLE SYSTEM IN AN EFFORT
TO CORRECT THE SCRUBBER RECYCLE PUMP CAVITATION PRO-
BLEMS.  THE VALUES DISPLAYED IN THE ACCOMPANYING TABLE
INCLUDE THE ACTUAL BOILER HOURS AND THE MODULAR OPER-
ATING HOURS.  THE PERFORMANCE INDEX VALUES CALCULATED
ARE BASED UPON TOTAL SCRUBBING SYSTEM OPERATION.

TESTS CONDUCTED THIS MONTH SHOWED THAT THE FGD  SYSTEM
MIST ELIMINATORS ARE NOT PERFORMING TO DESIGN AND THAT
THERE IS EXCESSIVE WATER ENTRAINED IN THE CLEANED FLUE
GA5SES CAUSING A STACK RAIN PROBLEM.  CHEMICO IS WORK-
ING ON THE DESIGN OF ADDITIONAL MIST ELIMINATORS THAT
WILL REMOVE THIS EXCESS WATER.  THE VENDOR is STILL
TRYING TO SOLVE THE REHEAT BURNER PROBLEMS.

SECONDARY VERTICAL MIST ELIMINATORS WERE INSTALLED IN
THE ABSORBER DISCHARGE DUCT IN AN ATTEMPT  TO REDUCE  THE
EXCESSIVE ENTRA1NEU WATER.  THEY DID NOT WORK BECAUSE
THE FLUE GAS BLEW THEM APART IN A FEW MINUTES OF OP-
ERATION.
          DURING A THREE WEEK OUTAGE (DUE TO A FURNACE  IMPLOSION)
          THE UNIT NO. 1 CHIMNEY FLUES WERE INSPECTED.   THE  'A'
          FLUE POLYESTER LINING MATERIAL WAS FLAKING  UFF  AND ACID
          ATTACK WAS STARTING TO CORRODE THE CARBON STEEL  FLUE.
          THE LINING VENDOR IS INVESTIGATING THE PROBLEM,  DURING
          THE OUTAGE THE PLUGGED MIST ELIMINATORS  WERE  CLEANED
          AND THE SCALE THROUGHOUT THE FtO SYSTEM  WAS REMOVED.
                                                  116

-------
PENNSYLVANIA  POWER CO.
MONTH  BOILER
OPERATING HOURS
  FGD MODULES
 B    C    0    E
                                                                  BRUCE  MANSFIELD  UNIT NO. 1
                                                                  COMMENTS
DEC. 76  732   584  726  664  433
TOTAL SYSTEM AVAILABILITY = 100X
TOTAL SYSTEM OPERABILITY =  100X
TOTAL SYSTEM RELIABILITY =  100*
TOTAL SYSTEM UTILIZATION =  971
                                         626
                                                     1 17

-------
PENNSYLVANIA POWER CO.                                           BRUCE MANSFIELD UNIT NO.  1

MONTH          BOILER                    F6D  MODULE
                           A      8       C       0       E       F

JAN. 77
OPERATING HOURS  675      660    613     502     661     627     614
FGO SYSTEM AVAILABILITY X  95     92      77      95      92      91
FGD SYSTEM OPERABILITY X   98     91      74      98      93      91
F6D SYSTEM UTILIZATION X   69     82      68      89      84      83
TOTAL FGD SYSTEM LOST GENERATION FACTOR*  =  11X
       DURING THE FIRST PART OF THE MONTH,  THE  THICKENER RAKE MECHANISM JAMMED AND COULD NOT BE RE-
       PAIRED.  THE THICKENER WAS OPERATED  FOR  APPROXIMATELY  THREE  WEEKS WITH THE RAKE STOPPED UNTIL
       THE UNIT NO. 2 THICKENER COULD BE  PUT  INTO EMERGENCY  SERVICE.   SEVERE WINTER WEATHER MADE
       OPERATION OF THE OUTDOOR FGD SYSTEM  VERY  DIFFICULT  AND AFFECTED THE RELIABILITY OF THE UNIT.

FEB. 77
OPERATING HOURS  540     437    376      439     516     544     451
FGD SYSTEM AVAILABILITY X  77     69      77      86      92      81
FGD SYSTEM UPERABILITY X   81     70      81      96     100      84
FGO SYSTEM UTILIZATION X   65     56      65      77     81      67
TOTAL FGO SYSTEM LOST GENERATION FACTOR  = 24.3X
       A SECOND SET OF VERTICAL SECONDARY M1S1  ELIMINATORS  WAS INSTALLED IN THE ABSORBER DISCHARGE
       DUCT BUT THE FLUE GAS BLEW THEM OUT  BEFORE THEIR EFFICIENCY  FOR REMOVING ENTRAINED WATER IN
       THE FLUE GAS COULD BE TESTED.

MAR. 1 THRU 12, 77
OPERATING HOURS  264      259    264     152     252     257     202
FGD SYSTEM AVAILABILITY X  99    100      58      95      97      80
FGD SYSTEM UPERABILITY X   98    100      58      95      97      77
FGD SYSTEM UTILIZATION X   98    100      58      95      97      77
TOTAL FGD SYSTEM LOST GENERATION FACTOR  = 12X
       AT 0000 MARCH  12TH THE UNIT WAS SHUT  DOWN FOR  A  10-WEEK TURBINE OVERHAUL OUTAGE.  DURING THE
       UUTA&E, REPAIRS WERE STARTED ON "A"  CHIMNEY  FLUE WHICH WILL  NOT BE  COMPLETED UNTIL THE END OF
       AUGUST.  AN INSPECTION OK "B" CHIMNEY  FLUE SHOWED THE  SAME TYPE OF  REPAIRS WOULD BE NEEDED,
       BUT WORK WILL  NOT START ON "6" UNTIL  THE  "A" FLUE HAS  BEEN REPAIRED.  BECAUSE OF THESE RE-
       PAIRS, THE UNIT WILL BE OPERATING  AT  APPROXIMATELY  HALF LOAD FUR ROUGHLY ONE YEAR.

MAR. 13 THRU MAY 22,  77
OPERATING HOURS             000       000
TOTAL FGO SYSTEM LOST GENERATION FACTOR  IS  DEFINED  AS  THE  TOTAL  MONTHLY LOST GENERATION DUE TO FGD
TRAIN OUTAGES DIVIDED BY THE T01AL MONTHLY  EXPECTED GENERATION IF THE FGD  TRAINS WOULD HAVE BEEN
AVAILABLE FOR OPERATION, EXPRESSED AS A  PERCENTAGE.
       BECAUSE OF THE EXCESSIVE MAINTENANCE  REQUIRED  ON THE  RUBBER  LINED CARBON STEEL I.D. FAN HOUS-
       INGS, FROM PIECES OF SCRUBBER SCALE  DAMAGING THE LINING AND  CORROSION OF THE CARBON STEEL,
       INCONEL PLATE  WILL BE INSTALLED ON THE SCROLL  AREA  OF  EACH OF  THE SIX FANS DURING THE OUTAGE.
       A NEWLY DESIGNED SECONDARY VERTICAL  MIST  ELIMINATOR  WILL  BE  INSTALLED IN THE ABSORBER DIS-
       CHARGE DUCT OF ONE OF THE SCRUBBER MODULES DURING THE  OUTAGE.
       DURING,THE OUTAGE, ALL SCRUBBING  VESSELS, DUCTS, PIPING AND  MIST ELIMINATORS WILL BE CLEANED
       AND ALL THE SCALE REMOVED.
       DURING OPERATION OF THE FGU SYSTEM,  THE  PH CONTROL  CUULD  NOT BE AUTOMATED BECAUSE OF POOR DE-
       SIGN AND OPERATIONAL PROBLEMS WITH THE PROVIDED  CONTROL SYSTEM.  PH CONTROL WAS MANUALLY
       SAMPLED AND CONTROLLED OVEK APPROXIMATELY UNE  YEAR  OF  OPERATION.  THE PH CONIRQL AND MONITOR-
       ING SYSTEMS ARE BEING REVISED BY  OPERATING PERSONNEL  DURING  THE OUTAGE IN AN EFFORT TO IM-
       PROVE THE PH CONTROL SYSTEM.
       THE LIME ADDITION PIPING IS BEING  REVISED IN EACH OF  THE  SCRUBBER VESSELS DUE TU THE SEVERE
       SCALING OCCURRING WITH THE CURRENT LIME  ADDITION SYSTEM.   ALSO THE  VENDOR IS REDESIGNING THE
       EXISTING MIST  ELIMINATOR SPRAY PIPING  IN  AN  EFFORT  TO  CORRECT  THE EXCESSIVE SCALING AND PLUG-
       GING OF THE MIST ELIMINATORS.
       CHANGES IN FLUSH WATER AND SEAL WATER  PIPING ARE BEING MADE  IN AN EFFORT TO CLOSE THE WATER
       LOOP.
       NEWLY MODIFIED REHEAT BURNERS WILL BE  INSTALLED  DURING THE OUTAGE AND TESTED ON "B" REHEATEK
       WHEN THE UNIT  STARTS UP IN MAY.
       THE UNIT NO. 1 THICKENER WAS CLEANED  OUT  AND THE JAMMED RAKE DRIVE  MECHANISM WAS REPAIRED
       DURING THE OUTAGE.

MAY 23 THRU 31, 77
OPERATING HOURS  121      0       00      102     103      50
FGD SYSTEM AVAILABILITY X                       100     100      47
FGO SYSTEM UPERABILITY X                         84      85      41
FGO SYSTEM UTILIZATION X                         47      48      23
TOTAL SYSTEM LOST GENERATION FACTOR = 87.2%
       UNIT WAS STARTED UP ON MAY 23RD,  USING D, E, AND F  MODULES,  DUE TO  REPAIRS BEING MADE TO "A"
       CHIMNEY FLUE.  HAD PROBLEMS SLAKING  LIME  A.MO GETTING  MAGNESIUM LEVELS BUILT UP IN THE SCRUB-
       BER RECYCLE LOOPS AFTER STARTUP.
                                                  118

-------
PENNSYLVANIA  POWER CO.

MONTH           BOILER
                                        FGD MODULE
                                         C      0
                                                                BRUCE MANSFIELD UNI I
JUN.  77
OPERATING  HOURS  669
F60 SYSTEM AVAILABILITY X
FGD SYSTEM OPERABILITY X
FGD SYSTEM UTILIZATION X
                                               676
                                                94
                                               100
                                                94
685
 95
100
 95
646
 90
 97
 90
TOTAL FGD SYSTEM LOST GENERATION FACTOR  =  53.7X
       HORIZONTAL MIST ELIMINATOR PRESSURE  DROPS  INCREASED TO THE POINT THAT NEW MIST ELIMINATOR
       MODULES WERE INSTALLED ON 0,E  AND F  SCRUBBERS AND D AND E ABSORBERS.  THE ONLY OUTAGES EXPER-
       IENCED BY THE UNIT THIS MONTH  WERE  DUE  TO  THE FGD SYSTEM.
JUL. 77
OPERATING HOURS  473
FGD SYSTEM AVAILABILITY X
FGD SYSTEM OPERABILITY X
FGO SYSTEM UTILIZATION X
                                               190
                                                99
                                               100
                                                66
193
 99
100
 66
471
 100
100
 63
 TOTAL FGD SYSTEM LOST GENERATION FACTOR  =  50.5X
       UNIT NO. 1 WAS DUWN FROM JULY  1ST THRU  JULY  12  TO MAKE SOME MODIFICATIONS TO THE GENERATOR
       COOLING SYSTEM.  ON JULY 19TH  AND 20TH, PENNSYLVANIA'S DEPARTMENT OF ENV1RUNMENTAL RESOURCES
       TESTED THE S02 AND PARTICULATE  EMISSIONS  FROM UNIT NO. 1'S FGD SYSTEM.   S02 EMISSIONS WERE
                                                                                   FGD so2 REMUVAL
       0.44 LB  S02/MM  BTU  AND  1.26 LB S02/MM 8TU FOR THE TWO TESTS RESPECTIVELY.
       EFFICIENCY  VARIED FROM  78X TO 89X FOK THE MONTH.

AUG.  77     692           3S3     373    210    692    689    635
FGO  AVAILABILITY  FACTOR  X   56      54     31     96      95    86
FGO  OPEHABILITY FACTOR X    57      56     31    100     99     95
FGO  UTILIZATION FACTOR X   52     50      28     93     93     85
TOTAL FGD  LOST  GENERATION  FACTOR = 32.5X
       UNIT NO. 1  WAS  DOWN FROM AUGUST 13 TO 15 BECAUSE OF BOILER TUBE LEAKS.  ON AUGUST 16, 1A
       CHIMNEY  FLUE  LINER  REPAIRS WERE COMPLETED AND A, B AND C TRAINS WERE STARTED UP.  SEVERAL
       REPAIRS  WERE  MADE TO THE ID FAN HOUSINGS THIS MONTH.  THE AVERAGE S02 REMOVAL EFFICIENCY FOR
       THE MONTH  WAS 86.7X GASED ON THREE GRAB SAMPLES.  YORK RESEARCH BEGAN SETTING UP TO CONTIN-
       UOUSLY MONITOR  THE  S02  REMOVAL EFFICIENCIES AS PART OF AN EPA RESEARCH PROJECT TO DETERMINE
       FEASIBLE NSPS FOR FGO.   EXTENSIVE MODIFICATIONS ARE BEING MADE IN THE PH CONTROL SYSTEMS
       IN  AN EFFORT  TO DEVISE  A WORKABLE PH CONTROL SYSTEM.

SEP.  77     558           543     528    545    334    314    245
FGO  AVAILABILITY  FACTOR  X   87      82     81     53    50      43
F6D  OPERABILITY FACTOR X    97      95     98     60     56     44
FGO  UTILIZATION FACTOR X    75      73     76     46     44     34
TOTAL FGD  LOST  GENERATION  FACTOR = 44.5X
       A BOILER TUBE LEAK  CAUSED THE UNIT TO BE DOWN SEPTEMBER 10 TO 12.
                                                                           FROM SEPTEMBER 17  TO 22
       THE UNIT WAS DOWN  TO  INSTALL  RIGGING  IN 18  CHIMNEY  FLUE 10 BEGIN FLUE LINER REPAIRS.   Or  E
       AND F TRAINS WERE  OFF  THE  REMAINDER  OF  THE  MONTH.   THE AVERAGE S02 REMOVAL EFFICIENCIES FOR
       THE MONTH WERE 93.2X  BASED ON FOUR  GRAB SAMPLE TESTS.
 OCT.  77     720           690    729     649        000
 FGD  AVAILABILITY FACTOR x   93      98      67       o      o       o
 FGO  OPERABILITY FACTOR X     96    100      90       0      0       0
 FGO  UTILIZATION FACTOR X    93      98      67       0      0       0
 TOTAL FGO LOST GENERATION FACTOR  = 55.4X
       CLEANED MIST ELIMINATOR  NOZZLES  AND MIST  ELIMINATOR ON "C".   ABS STACK REPAIRS ON UNIT  2
       NECESSITATED TAKING  UNIT  1  DOWN  FOR 2  DAYS.  (A PROTECTIVE CAP HAD TO BE PUT OVER 28 FLUE BY
       HELICOPTER.  PREVAILING  WINDS  NECESSITATED TAKING UNIT 1  OFF IN URDER TO DO THIS.)
                                                  119

-------
                  TABLE 3
PERFORMANCE DESCRIPTION FOR OPERATIONAL F6D  SYSTEMS  THROUGH
                                                             01/78
UTILITY NAME

UNIT NAME

UNIT LOCATION

UNIT RATING

FUEL CHARACTERISTICS

FGD VENDOR

PROCESS

NEW OR RETROFIT

START UP DATE

FGD STATUS

EFFICIENCY,
 PARTICULATES
                       PENNSYLVANIA POWER  co.

                       BRUCE MANSFIELD NO.  a

                       SHlPPINGPORT PENNSYLVANIA

                        825 MW

                       COAL «.7 PERCENT SULFUR

                       CHEMICO

                       LIME SCRUBBING

                       NEW

                        7/77

                       OPERATIONAL


                       99,8 PERCENT  (DESIGN)
 SO?
                       92  PERCENT  (DESIGN)
WATER MAKE UP
                      OPEN LOOP
SLUDGE DISPOSAL
                       RESERVOIR  LANDFILL
UNIT COST
                     SEE APPENDIX  A, FGO SYSTEM ECONOMICS
OPERATIONAL
 EXPERIENCE
                        REFER  TO  THE  BACKGROUND  INFORMATION  SECTION  IN  TABLE  3 OF THIS REPORT.
                        THIS EMISSION CONTROL  SYSTEM  WAS  DESIGNED  TO REMOVE FLYASH AND SOa FROM
                        3.35 MM ACFM  OF  FLUE GAS  USING  THIOSOKBIC  LIME  AS A SCRUBBING ABSORBENT.
                        SIX SCRUBBING TRAINS,  EACH  INCLUDING TWO  VENTURI  SCRUBBERS IN SERIES
                        ARRANGEMENT,  ARE PROVIDED FOR FULL-LOAD OPERA110N.   THE INITIAL SHAKEDOWN
                        AND DEBUGGING PHASE OF OPERATION  BEGAN FOR THREE  TRAINS IN JULY, 1977.
                        FULL COMMERCIAL  OPERATION FOH THE ENTIRE  SYSTEM COMMENCED ON OCTOBER 1,
                        1S77.
                                               120

-------
                                       BACKGROUND  INFORMATION
                                                 ON
                                     BRUCE MANSFIELD  UNIT  NO.  2

     THE  BRUCE  MANSFIELD PLANT IS A 2475 NET MW, THREE-UNIT, COAL-FIRED  FACILITY  LOCATED  ON  THE OHIO
RIVER IN  THE  BOROUGH OF SHIPPINGPORT, PENNSYLVANIA.   THIS  NEW  FACILITY  IS  BEING BUILT  BY  PENNS-
LVANIA  POWER  COMPANY,  ACTING ON ITS OWN BEHALF AND AS  AGENT  FOR  THE  OTHER  PARTICIPATING CENTRAL AKEA
POWER COORDINATION (CAPCO) GROUP OF INVESTOR-OWNED ELECTRIC  UTILITIES,  INCLUDING  THE  CLEVELAND ELEC-
RIC ILLUMINATING COMPANY, DUOUESNE LIGHT COMPANY,  OHIO  EDISON COMPANY,  AMD  TOLEDO  EDISON COMPANY
BRUCE MANSFIELD NO.  2,  WHICH IS IDENTICAL TO THE NO.  1 UNIT, IS  A  COAL-FIRED,  ONCE-IHKOUGH,  SUPER-
CRITICAL  STEAM  GENERATOR WHICH FIRES 333 TONS/HR OF COAL GENERATING  APPROXIMATELY 6.5  MM  LB/HR STEAM
AT 3,785  PSIG,  1005  F/1005 F.  THE EMISSION CONTROL EQUIPMENT  REQUIRED  FOR THIS UNIT  IS DESIGNED  TO
MEET STATE EMISSION  REGULATIONS OF 0.6 LBS SULFUR  DIOXIDE/MM BTU OF  HEAT INPUT AND  0.0175 GR/SCF  OF
PARTICULATE WHEN BURNING 11,900 8TU/LB COAL HAVING AVERAGE ASH AND SULFUR  CONTENTS  OF  12.5 AND
a.7 PERCENT,  RESPECTIVELY.

     IN LATE  1970, AN INTENSIVE INVESTIGATION OF MORE  THAN 30  POTENTIAL  DESULFURIZATIOM SYSTEMS WAS
INITIATED.  THE SYSTEM ULTIMATELY CHOSEN FOR THE REMOVAL OF  FLY  ASH  AND  SULFUR DIOXIDE WAS THE
VENTURI WET-SCRUBBING SYSTEM, PROVIDED BY CHEMICO  AIR  POLLUTION  CONTROL  CO.,  UTILIZING THE ORAVO
CORPORATION'S THIOSORBIC LIME AS THE SCRUBBING ABSORBENT.

     THE DESIGN FEATURES OF THE SCRUBBING SYSTEM DICTATE THAT  EACH SCRUBBING  TRAIN  CONSIST OF A
SCRUBBING VESSEL  (VARIABLE-THROAT VENTURI), A 9000HP  I.D.  FAN, AND AN  ABSORBER VESSEL  (FIXED-THROAT
VENTURI).  THERE ARE SIX SCRUBBER TRAINS PER UNIT  TO  HANDLE  THE  FLUE GAS FLOW  FROM  EACH BOILER AT
FULL LOAD (3.35 MM ACFM AT 285 F).  THE SCRUBBER/ABSORBER  TRAINS ARE ARRANGED  IN  GROUPS OF THREE.
THE  TREATED FLUE GAS, WHICH HAS PASSED THROUGH EACH GROUP  OF THE SCRUBBING SYSTEM TRAINS  IS  DUCTED
THROUGH ONE OF  THE TWO MEAT CHAMBERS AND THEN DISCHARGED FROM  ONE  OF iwo CHIMNEY  FLUES.   THE 950
FOOT CHIMNEY CONTAINS FOUR CARBON STEEL FLUES, THE INNER SURFACES  OF WHICH ARE COATED  WITH POLYESTER
FLAKEGLASS LINING AND ARE CAPABLE OF ACCOMMODATINGTWO  UNITS  AT FULL  LOAD.

     THE ADJUSTABLE VENTURI THROAT SCRUBBING MODULES  REMOVE  MOST OF  THE  FLYASH CONTAINED  IN  THE FLUE
GAS.  THE ABSORBER MODULE, WHICH IS A FIXED-THROAT VENTURI,  REMOVES  SOME OF  THE REMAINING FLYASH.
SULFUR DIOXIDE IS ABSORBED IN BOTH THE SCRUBBER  AND ABSORBER BY  DROPLETS OF  LIME  SLURRY,  CONTAINING
Z  TO 6 PERCENT MAGNESIUM OXIDE.

     THE SCRUBBER-RECYCLE BLEED IS COMBINED WITH A FLYASH  SLURRY FROM  THE  BOILER  AND  DISCHARGED TU A
200-FOOT DIAMETER THICKENER.  SLUDGE FROM THE THICKENER  IS THEN  PUMPED  TO  A  WASTE DISPOSAL SYSTEM
WHERE  IT  IS MIXED WITH A STABILIZING AGENT  (CALCILOX)  AND  THEN PUMPED  APPROXIMATELY 7  MILES  TO THE
LITTLE BLUE RUN DISPOSAL AREA.  THE DISPOSAL AREA  IS  LOCATED  IN A RAVINE  UPSTREAM  OF  A 400  FT HIGH
HYDRAULIC DAM DESIGNED TO CONTAIN THICKENER SLUDGE AND WATER.

     A SIMPLIFIED PROCESS FLOW DIAGRAM IS PRESENTED IN APPENDIX  8.
 INFORMATION CONCERNING THE PERFORMANCE OF THE UNIT SINCE COMMERCIAL  OPERATIONS COMMENCED  IN  OCTOBER
 1977 ARE  SUMMARIZED AND  PROVIDED IN THE TABLE THAT  FOLLOWS.
                                                  121

-------
PENNSYLVANIA POWER CO.
                                                                     BRUCE MANSFIELD  UNIT  NO.  2
                                 OPERATING HOURS
                                    F6D MODULES
MONTH     BOILER
                         A      6       CD       E       F
OCT. 77     595         621    652     645    361     3«9     305
F6D AVAILABILITY FACTORX 9M     97      98     63      66      61
FGO OPERABILITY FACTORX 100    100     100     61      59      51
FGD UTILIZATION FACTORX  83     88      87     48      47      41
TOTAL FGD LOST GENERATION FACTOR 25.7X                                                        .,,-.»
       UNIT 2 WAS DECLARED AVAILABLE FOR COMMERCIAL OPERATION AT 825 MK ON OCTOBER Ir  1977.   CLEANED
       SPRAYS IN 2F FAN.  REPAIRS BEING MADE TO 2B FLUE STACK LINING DUE TO PREMATURE  FAILURE OF
       SEVERAL TEST PATCHES.  UNIT TRIPPED DUE TO FAULTY GENERATOR CONTROL TRANSFORMERS.
                                                  122

-------
                  TABLE 3
PERFORMANCE DESCRIPTION FOR OPERATIONAL  FGD  SYSTEMS  THROUGH  01/76
 UTILITY NAME


 UNIT NAME


 UNIT LOCATION


 UNIT RATING


 FUEL CHARACTERISTICS


 FGD VENDOR


 PROCESS


 NEW OR RETROFIT


 START UP DATE


 FGD STATUS


 EFFICIENCYr
  PARTICIPATES
PHILADELPHIA ELECTRIC CO.


EODYSTONE NO. 1A


EDOYSTONE PENNSYLVANIA


 12U MM


CUAL 2.b PERCENT SULFUR


UNITED ENGINEERS / PECO


MAGNESIUM OXIDE SCRUBBING


RETROFIT


 9/75


OPERATIONAL



99.9 PERCENT
   S0£
                        90  PERCENT
  WATER MAKE UP
                        OPEN  LOOP  1.1  GPM/MW
  SLUDGE DISPOSAL
                        ACID  PLANT  REGENERATION
  UNIT COST
                       SEE  APPENDIX  A,  FGO  SYSTEM ECONOMICS
  OPERATIONAL
   EXPERIENCE
REFER TO THE BACKGROUND  INFORMATION SECTION IN TABLE 3 OF THIS REPORT.
THE EMISSION CONTROL SYSTEM FOR THIS UNIT CONSISTS OF THREE PARALLEL
SCRUBBING  TRAINS FOR THE CONTROL OF PARTICULATE AND SULFUR DIOXIDE.
THE C-SIDE SCRUBBING TRAIN INCLUDES AN S02 ABSORBER MODULE IN SERIES
WITH A PARTICULATE SCRUBBER. APPROXIMATELY ONE-THIRD OF THE BOILER FLUE
GAS IS SCRUBBED WITH MAGNESIUM OXIDE SLURRY FOR S02 REMOVAL. THE SPENT
SLURRY is  REGENERATED  AT THE ESSEX SULFURIC ACID PLANT IN NEWARK, N.J.
THE REGENERATED MAGOX  IS RETURNED TO THE PLANT FOR SOt! SCRUBBING SERVICE.
                                               123

-------
                                       BACKGROUND  INFORMATION
                                                 UN
                                           EDDYSTONE MO.  1

     THE EDDYSTONE STATION OF THE PHILADELPHIA ELECTIRC CO.  (PECO)  IS  LOCATED  ON  THE  DELAWARE RIVER
IN EDUYSTONE, PENNSYLVANIA, ABOUT 11 MILES SOUTHWEST OF THE  CENTER  OF  PHILADELPHIA.   THE PLANT IS
APPROXIMATELY FIVE MILES WEST OF ONE OF THE MAIN RUNWAYS  OF  THE PHILADELPHIA  INTERNATIONAL AIRPORT.

     THE STATION HAS FOUR GENERATORS WITH A TOTAL  NET GENERATING CAPACITY  OF  1370  MW.   UNITS 1 AND 2
BURN COAL WITH AN AVERAGE GROSS HEATING VALUE OF 18,100 BTU/LB AND  ASH  AND  SULFUR  CONTENTS OF
12 PERCENT AND 2.3 PERCENT, RESPECTIVELY.  STEAM CONDITIONS  ARE 5,000  PSI  AND  1150  f.   THESE ARE THE
HIGHEST UTILITY PLANT OPERATING PRESSURE AND TEMPATURE CONDITIONS IN THE UNITED STATES.
UNITS 1 AND 2 ARE BASE-LOAD UNITS.  UNITS 3 AND It  ARE PEAK-LOAD GENERATORS  WHICH  BURN  NO.  6 OIL.

     THERE ARE TWO FURNACES ON THE UNIT 1 BOILER.  EACH FURNACE WAS INSTALLED  WITH  PARTICULATE CONT-
ROLS CONSISTING OF MECHANICAL COLLECTORS AND AN ELECTROSTATIC PREC1PITATOR.

     THE MAGNESIUM OXIDE-BASED FLUE GAS DESULFURIZATION (FGD) SYSTEM ON BOILER NO.  1  AT  THE EDDY-
STONE STATION OF PHILADELPHIA ELECTRIC COMPANY IPECO)  WAS DESIGNED AND INSTALLED  BY  UNITED ENG-
INEERS AND CONSTRUCTORS, INC., IN CO-OPERATION WITH PHILADELPHIA ELECTRIC.  THE SYSTEM CONSISTS OF
THREE FIRST-STAGE SCRUBBER MODULES IN PARALLEL FOR PARTICULATE CONTROL  (TWO ENVIRONEERING  VENTURI
ROD UNITS AND ONE PEABOOY-LURGI VENTURI UNIT) AND  A SECOND-STAGE ENVIRONEERING ABSORBER  MODULE WITH
TWO VENTURI-ROD bEDS FOR SULFUR DIOXIDE REMOVAL.

     THfc THREE FIRST-STAGE SCRUBBERS TOGETHER ARE  SIZED TO HANDLE ALL  THE  EXHAUST  GAS  FROM UNIT
1 WHICH HAS A NET ELECTRIC GENERATING CAPACITY OF  316 MW.  THE SECOND-STAGE ABSORBER  IS  SIZED TO
HANDLE ONE-THIRD OF THE GAS FLOW, EQUIVALENT TO APROXIMATELY 105 MW (NET).  THE SYSTEM IS  DESIGNED
TO REMOVE 90 PERCENT OF THE SULFUR DIOXIDE FROM BOILER STACK GAS.   A GENERAL PROCESS FLOW  DIAGRAM
OF THE WET SCRUBBING SYSTEM IS PRESENTED IN APPENDIX B.
SCRUBBER OPERATING HISTORY

     THERE WAS A BRIEF OPERATING PERIOD ON THE PARTICULATE SCRUBBERS FROM MID-NOVEMBER,  1974 TO
MARCH, 1975, THAT UNCOVERED A NUMBER OF PROBLEM AKEAS.  DUE  TO A NUMBER OF EXTENUATING CIRCUM-
STANCES, PARTICULATE SCRUBBING WAS NOT RESTARTED UNTIL JULY  23, 1975,  WITH ONE PARTICULATE SCRUBBING
TRAIN FOLLOWED BY THE OTHER TWO TRAINS, ON AUGUST  15 AND  OCTOBER 2, RESPECTIVELY.   THE SULFUR
DIOXIDE ABSORBER WAS STARTED FOR THE FIRST TIME ON OCTOBER 2, 1975, AND THE MAGNESIUM  OXIDE REGEN-
ERATION FACILITY FIRST PROCESSED MAGNESIUM SULFITE FROM THE  EODYSTONE  SCRUBBER ON OCTOBER  28,  1975.

     THE MAGNESIUM OXIDE REGENERATION FACILITY HAS BEEN OPERATED TO PROCESS ALL MAGNESIUM  8ULFITE
DOWNS AT THE E&OYSTONE SCRUBBER.

     THE SULFUR DIOXIDE SCRUBBING SYSTEM WAS TEMPORARILY  SHUT DOWN DECEMBER 31, 1975,  BECAUSE THE
ACID PLANT REGENERATION FACILITY AT THE OLIN CHEMICAL SULFURIC ACID PLANT  IN PAULSBORO,  NEW JERSEY
PERMANENTLY CEASED OPERATIONS.  THE ACID PLANT REGENERATION  FACILITY WAS RELOCATED  TO  THE  ESSEX
CHEMICAL PLANT IN NEWARK, NEW JERSEY.
     THE PARTICULATE AND SULFUR DIOXIDE REMOVAL SYSTEM INSTALLED ON THE EDOYSTONE NO.  1  UNIT IS THE
FIRST PHASE OF A TWO-PHASE PROJECT.  FOLLOWING SUCCESSFUL DEVELOPMENT  OF THIS  SYSTEM WITH  MORE CONT-
INUOUS OPERATION, IT WILL BE INCORPORATED INTO THE DESIGN FOR THE COMPLETE SULFUR DIOXIDE  REMOVAL  ON
EDDYSTONE NO. 2 AND ONE OF THE TWO EXISTING UNITS  AT THE  CROMBY STATION.

     ADDITIONAL INFORMATION AND DATA CONCERNING THE OPERATION OF THE PAHTICULATE  AND SULFUR DIOXIDE
SCRUBBERS INSTALLED AT THIS PLANT ARE PROVIDED IN  THE PERFORMANCE TABLE THAT FOLLOWS.
                                                 124

-------
PHILADELPHIA  ELECTRIC CO.            FGD SYSTEM  PERFORMANCE           EDDYSTONE UNIT  NO.  1

PERIOD                                          COMMENTS
NOV.  7tt    THE SCRUBBING SYSTEM AT THIS PLANT  CONSISTS  OF  THREE PARALLEL SCRUBBING TRAINS  INCOR-
DEC.  74    PORATING 3 KET PARTICULATE SCRUBBERS AND  ONE  302 ABSORBER MODULE.   THERE WAS  A  BRIEF
JAN.  75    OPERATING PERIOD ON THE PARTICULATE SCRUBBERS FROM MIO-NOVEMBER 1974 TO MARCH 1975
FEB.  75    PROBLEMS ENCOUNTERED CENTERED AROUND THE  SCRUBBER BOOSTER FANS AND  THt FLUE SAb  AMU LlUUin
MAR.  75    CONDITIONS.  THE B-SIDE BOOSTER FAN DEVELOPED HIGH SHAFT  VIBRATION  WHEN STARTtD  FOR THE
APR.  75    FIRST TIME.  THIS PROBLEM WAS DESIGN-RELATED, INVOLVING AN EXCESSIVE CLEARANCE  AREA
MAY  75    BETWEEN THE SHAFT AND THE WHEEL HUB.  ALSO,  EXTENSIVE CORROSION DEVELOPED IN  THE  C-SIDE
JUN.  75    PARTICULATE SCRUBBER INTERNALS.   THIS  WAS CAUSED BY LOW SCRUBBING  SOLUTION  PH LEVELS AND
          CHLORIDE LEVELS AS HIGH AS 2000 PPM.  THESE  CONDITIONS COUPLED WITH THE THERMAL  SHOCK  OF A
          HOT START PROCEDURE CAUSED THE CORROSION.  THIS PROBLEM WAS AMELIORATED BY  CAUSTIC  AD-
          DITION, HIGHER 6LOWDOWN AND EMPLOYING  A  COLD  START PROCEDURE.  AT  APPROXIMATELY  THIS TIME,
          A CHECKOUT OF S02 SYSTEM WAS CONDUCTED.   BLISTERING AND PEELING OF  THE POLYURETHANE
          COATINGS WERE DETECTED AND CORRECTED BY  RECOATING WITH FLAKE GLASS.

JUL. 75    THE C-SIDE PARTICULATE SCRUBBER RESTARTED ON  JULY 23, 1975.  THE TWO REMAINING  TRAINS, B-
AU6. 75    SIDE AND A-SIOE, WERE PUT INTO OPERATION  ON  AUGUST 15 AND OCTOBER  2, RESPECTIVELY.  THE
SEP. 75    SU2 ABSORBER MODULE IN THE C-SIDE SCRUBBING  TRAIN WAS INITIALLY PLACED IN SERVICE OCTOBER
OCT. 75    2,  1975.  THE OLIN CHEMICAL MGO REGENERATION  FACILITY FIRST PROCESSED MAGNESIUM  SULFITE
NOV. 75    FROM THE EDOYSTONE SCRUBBER ON OCTOBER 28,  1975.  THE C-SIDE PARTICULATE SCRUbBER OPERATED
DEC. 75    A TOTAL OF 2831 HOURS THROUGH JANUARY  31, 1976, FOR AN AVAILABILITY OF 70 PERCENT.  THE
JAN. 76    B-SIDE TRAIN HAS OPERATED A TOTAL OF 1933 HOURS THROUGH JANUARY 31, 197b FOR  AN  AVAIL-
          ABILITY OF 55 PERCENT.  THE A-SIDE  TRAIN  OPERATED A TOTAL OF 626 HOURS THROUGH  JANUARY
          31, 1976, FOR AN AVAILABILITY OF  24 PERCENT.  THE C-SIDE  S02 ABSORBER WAS IN  SERVICE A
          TOTAL Of 556 HOURS THROUGH DECEMBER 31,  1975, WITH AN AVAILABILITY  OF 33 PERCENT  SINCE
          STARTUP.  PROBLEMS ENCOUNTERED IN THE  OPERATION OF THE THREE SCRUBBING TRAINS INCLUDED:
          UNDER-DESIGNED RECIRCULATION PUMPS, MALFUNCTION OF THE FLUE GAS BY-PASS DAMPER  DRIVE UNITS
          AND FAILURE OF THE OOUBLE-BRlCK REFRACTORY  LINING IN THE  REHEAT COMBUSTION  CHAMBER.

FEB. 76   OPERATION OF THE S02 SCRUBBING SYSTEM  AT  EODYSTONE WAS TEMPORARILY  HALTED BECAUSE THE  ACID
MAR. 76   PLANT REGENERATION FACILITY AT THE  OLIN  CHEMICAL SULFURIC ACID PLANT IN PAULSBORO,  NEW
 APR. 76   JERSEY PERMANENTLY CEASED OPERATIONS.   THE  UTILITY IS NOW INVESTIGATING ALTERNATIVE
MAY  76   REGENERATION SITES.  A MINUMUM PERIOD  OF  SIX  MONTHS WILL  BE REQUIRED FOR RELOCATION ONCE A
          CHOICE IS MADE.  THE UTILITY ANNOUNCED PLANS  FOR RELOCATION OF THE  REGENERATION  FACILITY
          AT THE ESSEX CHEMICAL PLANT IN NEWARK, NEW  JERSEY.

 JUN. 76   RESUMPTION OF S02 SCRUBBING OPERATIONS IS PRESENTLY SCHEDULED FOR  DECEMBER  1976.  THE
 JUL. 76   RELOCATION OF THE REGENERATION FACILITY  IS  NOW  IN PROGRESS.  THE PARTICULATE  SCRUBBERS ARE
 AUG. 76   OPERATIONAL.  THE C-SIDE  BOOSTER  FAN HAS  DEVELOPED A MATERIALS FAILURE BETWEEN  THE  HUB AND
          SHAFT  (IDENTICAL TO THE B-SIDE UNIT MENTIONED ABOVE).

 SEP. 76   ALL THREE BOOSTER FANS HAVE NOW DEVELOPED THE MATERIALS FAILURE BETWEEN THE HUB  AND SHAFT
 OCT. 76   (AS IDENTIFIED IN THE ABOVE FOR THE B-SIDE  UNIT).  THESE  UNITS HAVE BEEN RETURNED TO THE
          MANUFACTURER FOR MODIFICATIONS AND  REPAIRS.   CURRENTLY, ONE OF THE  PARTICULATE  SCRUBBERS
          IS IN  THE FLUt GAS STREAM.  TO DATE, ALL  THREE  OF THE WET PARTICULATE SCRUBBERS  HAVE N01
          SEEN ANY APPRECIABLE SIMULTANEOUS SERVICE TIME.

 NOV. 76   MGO SCRUBBING OPERATIONS  ARt NOW  SCHEDULED  TO RESTART IN  MAY 1977.   REGENERATION  FACILITY
 DE.  76    RELOCATION IS BEING COMPLETED, AND  MODIFICATIONS TO THE ID BOOSTER  FANS CURRENTLY BEING
          EFFECTED CONSIST OF CONVERSION FROM A  SHRINK  FIT TO A SLIP FIT.  THESE MODIFICATIONS ARE
          EXPECTED TO ELIMINATE RECURRING VIBRATION PROBLEMS.

 JAN. 77   THE MAGNESIUM OXIDE SCRUBBING SYSTEM AT  EDDYSTUNE NO. 1A  IS STILL  SCHEDULED FOR  RESTART  IN
 FEB. 77   MAY 1977.  THE START-UP OF THE NEW  MAGNESIUM  SULFITE REGENERATION  FACILITY  AT THE ESSEX
 MAR. 77   CHEMICAL PLANT AT NEWARK, N.J. IS ALSO SCHEDULED FOR MAY  1977.  THE THREE PARALLEL  VEN1URI
          SCRUBBERS CONTROLLING PARTICULATE EMISSIONS  ON  EDOYSTONE  NO. 1 WENT BACK INTO SERVICE  IN
          MARCH  1977.

 APR. 77   RESUMPTION OF MAGNESIUM OXIDE SCRUBBING  OPERATIONS OCCURED DURING  THE REPORT  PERIOD.   THE
 MAY  77   UTILITY REPORTED THAT S02 SCRUBBING OPERATIONS  WERE NOT CONTINUOUS  THROUGHOUT THE PERIOD.
          THE ABSORBER WAS IN SERVICE APPROXIMATELY 206 HOURS DURING MAY.  REGENERATION OPERATIONS
          AT THE ESSEX FACILITY WERE NOT CONDUCTED  DURING THE PERIOD.  PECO  INTENDS TO  INITIATE  S02
          RECOVERY AND MAGOX REGENERATION OPERATIONS  OUKING THE MONTH OF JUNE.  THE S02 MODULE CON-
          TAINS TWO ABSORBER SECTIONS IN SERIES  (EACH  SECTION CONSISTING OF  AN ADJUSTABLE  ROD DECK
          WITH UNDERSPRAYS).  ONLY  ONE OF THE ABSORBER  SECTIONS IS BEING USED FOR 502  REMOVAL.  S02
          REMOVAL EFFICIENCY HAS NOT BEEN MEASURED.  MAGNESIUM UXIDE LOSSES  IN THE SYSTEM  (ABSOR-
          TION AND REGENERATION) ARE ESTIMATED AT  10  PERCENT.

 JUN. 77   FAILURE OF MINOR ANCILLARY EQUIPMENT CAUSED  SOME SHUTDOWNS.  LATER, THE BOILER  ITSELF  WENT
 JUL. 77   DOWN.  OVER THIS PERIOD THE ROTARY  VALVE  ON  THE MAG. SULFITE DRYER  DISCHARGE  PLUGGED
          REPEATEDLY   ALSO THE BELTS ON THE  AGITATOR  ON  THE MAG-OX. PRESLAKER FAILED.
                                                  125

-------
PHILADELPHIA ELECTRIC CO.            FGD SYSTEM PERFORMANCE      EDDYSTONE UNIT NO.  1

p£RIOO                                        COMMENTS

AUG. 77   THE ROTARY VALVE PROBLEM APPEARS TO BE SOLVED.  CUMULATIVE AVAILABILITY SINCE MAY  IS
SEP. 77   ESTIMATED TO BE ROUGHLY 33X.  PECO REPORTED 131 HOURS OF CONTINUOUS OPERATION FOR  THE
          SCRUBBER AND THICKENER CENTRIFUGE DRYER LOOP.  DURING THE REPORT PERIOD THERE HAVE BEEN
          CONTINUAL PROBLEMS WITH THE GLAND PACKING ON THE FGD SYSTEM CIRCULATION PUMPS (STUFFING
          BOX).  PECO HAS SINCE CHANGED THE GLANO CONFIGURATION.  THEME ALSO WAS A PROBLEM rtlTH HIGH
OCT. 77   SOLIDS FORMATION IN THE THICKENER.  DURING THE OCTOBER-NOVEMBER PERIOD THERE WAS ONE RUN
          WHICH LASTED APPROXIMATELY 5 DAYS.
NOV. 77   GLAND PACKING PROBLEMS PERSISTED AND MECHANICAL SEALS ARE BEING CONSIDERED AS POSSIBLE
          ALTERNATIVES.  EVEN WITH HEAT TRACING THE SEAL WATER FROZE-UP CAUSING ROTAMETERS TO BURST.
          HIGH SOLIDS PROBLEM IN THICKENER IS STILL A PROBLEM AREA.

DEC. 77   THE UNIT WENT DOWN DECEMBER 22 FOR A TURBINE OVERHAUL.  DURING THE OUTAGE MAINTENANCE AND
JAN. 78   MINOR MODIFICATIONS WILL BE MADE ON THE SCRUBBERS.   THE UNIT IS EXPECTED BACK ON LINE THE
          FIRST WEEK IN MARCH.  THE AVAILABILITY FACTOR FOR THE OCT,  NOV, AND DEC QUARTER WAS 4U.
          DURING THIS PERIOD SOME OF THE HEAT TRACING FAILED  AND OTHER PROBLEMS OCCUHED WHEN LINES
          FROZE AT THE ACID PLANT CAUSING THE FACILITY TO BE  RUN INTERMITTENTLY.  THE GLAND PACKING
          PROBLEMS HAVE NOT YET BEEN SOLVED AND MECHANICAL SEALS ARE STILL BEING CONSIDERED.
                                                 126

-------
                  TABLE 3
PERFORMANCE DESCRIPTION FOR OPERATIONAL  FGU  SYSTEMS THROUGH
                                                              01/78
 UTILITY NAME

 UNIT NAME

 UNIT LOCATION

 UNIT RATING

 FUEL CHARACTERISTICS

 F60 VENDOR

 PROCESS

 NEW OR RETROFIT

 START  UP DATE

 FGO STATUS

 EFFICIENCY,
  PAHTICULATES
 SOUTH CAROLINA PUBLIC SERVICE

 W1NYAH NO.  2

 GEORGETOWN  SOUTH CAROLINA

  260 MM

 COAL  1.0 PERCENT SULFUR

 BABCOCK & WILCUX

 LIMESTONE SCRUBBING

 NEW

  7/77

 OPERATIONAL


 99.4 PERCENT
                        35  PERCENT  (TOTAL)
  WATER MAKE UP
                        OPEN  LOOP
  SLUDGE DISPOSAL
  UNIT COST
  OPERATIONAL
   EXPERIENCE
SEE APPENDIX A, FGD SYSTEM ECONOMICS
 REFER TO THE BACKGROUND INFORMATION SECTION IN TABLE 3 OF THIS REPORT.
 THE EMISSION CONTROL SYSTEM FOR THIS UNIT CONSISTS OF A IOOX CAPACITY ESP
 FOLLOWED BY A SOX CAPACITY LIMESTONE FGO SYSTEM. ONE FGD MODULE, CONSIST-
 ING OF A VENTURI SCHUbBER AND TRAY TOrtER ABSORBER, REMOVES 70* OF THE
 INLET S02. REHEAT IS SUPPLIED BY THE FLUE GAS BYPASS. THE SCRUBBING
 WASTES ARE DISCHARGED TO AN ON-SITE, UNLINED DIKED POND. THE NO. i. UNIT
 COMMENCED INITIAL OPERATIONS IN JULY 1977. THE ACCEPTANCE TEST FOR COM-
 MERCIAL CERTIFICATION WAS SUCCESSFULLY COMPLETED IN DECEMBER 1977.
                                               127

-------
                                       BACKGROUND INFORMATION
                                                 ON
                                            WINYAH NO. 2

     THE SOUTH CAROLINA PUBLIC SERVICE AUTHORITY OWNS AND OPERATES THE WINYAH STEAM  PLANT  WHICH IS
LOCATED IN GEORGETOWN, SOUTH CAROLINA,  THIS NEW COAL-FIRED POWER-GENERATING STATION  CONSISTS  OF  TWO
OPERATIONAL UNITS AND ONE IN THE EARLY PLANNING STAGES.  UNITS NO. 1 AND NO. 2 ARE RATED AT  315 MW
AND 280 MW, RESPECTIVELY, AND FIRE A MEDIUM SULFUR VIRGINIA COAL WITH THE FOLLOWING  GENERAL  CHARAC-
TERISTICS: 11,200 BTU/LB, 1.9 PERCENT SULFUR (MAXIMUM), 19 PERCENT ASH (MAXIMUM)  AND  10 PERCENT
MOISTURE (MAXIMUM).  IN ORDER TO MEET FEDERAL NEW SOURCE PERFORMANCE STANDARDS FOR PARTICULATE  AND
SULFUR DIOXIDE EMISSIONS, UNIT NO. 2 IS FITTED WITH AN EMISSION CONTROL SYSTEM WHICH  INCLUDES  Ah
ELECTROSTATIC PRECIPITATOR (ESP) AND A WET SCRUBBING SYSTEM.  THE ESP, INSTALLED  UPSTREAM  OF THE
SCRUBBER-ABSORBER PLANT, IS SUPPLIED bY RESEARCH-COTTRELL AND DESIGNED TO REMOVE  APPROXIMATELY  99
PERCENT OF THE INLET FLY ASH.  THE WEI SCRUBBING SYSTEM CONSISTS OF A LIMESTONE BASED FGD  DESIGNED
AND SUPPLIED BY BABCUCK AND WILCOX TU REMOVE ADDITIONAL FLY ASH AND REMOVE 69 PERCENT Of THE SULFUR
DIOXIDE FROM 50 PERCENT OF THE FLUE GAS.  THE REMAAINING HALF OF THE BOILER FLUE  GAS  IS BYPASSED
AROUND THE FGD SYSTEM AND RECOMBINED WITH THE SCRUBBED PORTION FOR REHEAT PURPOSES PRIOR TO  DIS-
CHARGE TO THE STACK.

     THE FGD SYSTEM CONSISTS OF ONE SCRUBBER-ABSORBER TRAIN, INCLUDING A VENTURI  SCRUBBER  AND  TRAY
TOWER ABSORBER.  FOLLOWING PASSAGE UF THE FLUE tAS THROUGH THE ESP (0.1 LB/MM BTU DESIGN OUTLET
LOADING), 50 PERCENT OF THE FLUE GAS (<407,015 ALFM,  270 F) IS BOOSTED THROUGH THE SCRUBBER AND  ABSO-
RBER BY A DRY, FORCED-DRAFT BOOSTER FAN (DESIGN PRESSURE DROP OF 13.5 INCHES).  THE VENTURI  SCRUBBER
PROVIDES ADDITIONAL FLY ASH AND INITIAL SULFUR DIOXIDE REMOVAL.  THE DESIGN FEATUKES OF THE  VENTURI
INCLUDE A 3 INCH PRESSURE DROP, A SUPERFICIAL GAS VELOCITY OF 90 FT/SEC., AND L/G OF 1«.«.   THE SAT-
URATED FLUE GAS (338,000 ACFM, 126 F) THEN PASSES THROUGH THE TRAY TOWER WHERE SULFUR DIOXIDE
REMOVAL IS COMPLETED.  THE DESIGN FEATURES OF ThE ABSORBER INCLUDE A 4.5 INCH PRESSURE DROP, A
SUPERFICIAL GAS VELOCITY OF 10.5 FT./SEC., AND A L/G OF 07.5.  THE SCRUBBING SOLUTION is A 20 PER-
CENT SOLIOS LIMESTONE SLURRY FED TO THE FGD SYSTEM AT A 130 PERCENT STOICHIOMETRIC LEVEL.  THE  OVER-
ALL EMISSION CONTROL SYSTEM REMOVAL EFFICIENCY IS 99.55 PERCENT FOR PAftTICULATE AND 35 PERCENT  FOR
SULFUR DIOXIDE (935 PPM INLET AND 290 PPM OUTLET FOR THE FGD SYSTEM).  THE SCRUBBING WASTES  (6.45
TONS PER HOUR, 35 PERCENT SOLIDS) ARE DISCHARGED VIA PUMP TO AN ON-SITE,  UNLINED  DIKED POND  WITH A
20-YEAR CAPACITY.  THE CLEANED GASES ARE RECOMB1NED WITH THE BYPASSED PORTION AND DISCHARGED TO AN
FRP-LINED STACK.
                                                 128

-------
SOUTH CAROLINA PUBLIC SERVICE
                                      FGD  SYSTEM  PERFORMANCE
                                               COMMENTS
                                                           WINYAH  NO.  2
PERIOD
OCT. 77
NOV. 77

OEC. 77
JAN. 78
DURING UPDATE PERIOD THE  SCRUBBER  SYSTEM  WAS  OPERATIONAL  AND  AVAILABLE  1001  Of  THE TIME.


DURING THE UPDATE PERIOD,  THERE  WERE  NO FORCED OUTAGES  EXCEPT IN  EARLY  JANUARY  WHEN THE
SYSTEM WAS DOWN FOR TWO  DAYS  TO  CHECK THE INSTRUMENTATION.   THE  S02  MONITORS ARE  NOT
FUNCTIONING PROPERLY.   ALL  THE  SAMPLE LINES HAVE BEEN REPLACED SEVERAL  TIMES.   NEn HEAT
TRACINGS ARE  INSTALLED  AROUND THEM.   THE  ACCEPTANCE TESTS ARE EXPECTED  TO  BE OVER BY  THE
END OF FEB.
                                                   129

-------
                  TABLE 3
PERFORMANCE DESCRIPTION FOR OPERATIONAL FGD SYSTEMS THROUGH   01/78
 UTILITY NAME          SPRINGFIELD CITY UTILITIES

 UNIT NAME             SOUTHWEST NO.  1

 UNIT LOCATION         SPRINGFIELD MISSOURI

 UNIT RATING            200 MW

 FUEL CHARACTERISTICS  COAL 3.b PERCENT SULFUR

 FGD VENDOR            UNIVERSAL OIL  PRODUCTS

 PROCESS               LIMESTONE SCRUBBING

 NEW OR RETROFIT       NEW

 START  UP DATE          4/77

 FGD STATUS            OPERATIONAL

 EFFICIENCY,
  PARTICULATES         99.8 PERCENT  (ACTUAL)


  S02                  92 PERCENT  (ACTUAL)


 WATER  MAKE  UP


 SLUDGE DISPOSAL       FILTER CAKE LANDFILL


 UNIT COST            SEE APPENDIX A, FGD SYSTEM ECONOMICS


 OPERATIONAL           REFER TO THE  bACKGROUNO  INFORMATION SECTION  IN  TABLE  3 OF  THIS  REPORT.
  EXPERIENCE           THE EMISSION  CONTROL SYSTEM FOR THIS NEW COAL-FIRED UNIT CONSISTS  OF  A
                       FOUR-FIELD  HIGH EFFICIENCY ESP  (99.6X DESIGN) AND  2 TURBULENT CONTACT AB-
                       SORBER MODULES (SOX DESIGN) FOR THE CONTROL  OF  PARTICULATES  AND SOS.  BOTH
                       THE ESP AND LIMESTONE FGD SYSTEM ARE SUPPLIED BY UOP. THE  SCRUBBING
                       WASTES ARE  OEWATERED BY  A ROTARY DRUM VACUUM FILTER AND  THE  FILTER CAKE  IS
                       HAULED AWAY TO A LANDFILL. INITIAL OPERATION OF THE FGD  SYSTEM  OCCURRED  IN
                       APRIL 77. IN  SEPT. 77, THE UNIT SUCCESSFULLY COMPLETED COMPLIANCE  TESTING.
                                               130

-------
                                        BACKGROUND INFORMATION
                                                  ON
                                           SOUTHWEST NO. i

     THE  SOUTHWEST POWER STATION OF  THE CITY  UTILITIES OF  SPRINGFIELD IS LOCATED APPROXIMATELY FIVE
MILES SOUTHWEST OF SPRINGFIELD, MISSOURI.   THE  STATION NOW OPERATES ONE CUAL-FIREO STEAM TURBINF
GENERATOR,  WHICH HAS A TOTAL GENERATING CAPACITY OF 200 MW.  PLANS CALL FUR A SECOND COAL-FIRED
GENERATOR OF LIKE CAPACITY TO BEGIN  OPERATING IN 1981, WHICH WILL BRING THE STATION'S CAPACITY UP TO
UOOMW.

     THE  NO. 1 BOILER IS A RILEY STOKER PULVERIZED COAL-FIRED UNIT.  THE FUEL IS A HIGH-SULFUR BITU-
MINOUS KANSAS COAL WITH THE FOLLOWING  AVERAGE CHARACTERISTICT5: 10 PERCENT ASH,  3.5 PERCENT SULFUk,
AND 12,500 BTU/LB HEATING VALUE.   PRIMARY  PARTICULATE CONTROL IS PROVIDED BY A COLD-SIDE ELECTROS1A-
TIC PRECIPITATOR  (ESP) WITH AN  EFFICIENCY  OF  99.7 PERCENT, AND PRIMARY SULFUR DIOXIDE (SU2) EMISSION
CONTROL BY A LIMESTONE SLURRY FLUE GAS DESULFUR1ZAT ION (FGD) SYSTEM WITH A DESIGN EFFICIENCY OF BO
PERCENT.   THESE UNIVERSAL OIL PRODUCTS CONTROL  SYSTEMS ARE DESIGNED To MEET NEW SOURCE PERFORMANCE
STANDARDS OF 0.1  LB/MM BTU F02  PARTICULATES AND 1.2 LB/MM  BTU FU2.S02 EMISSIONS.

     THE FGD SYSTEM  INCLUDES TWO bO  PERCENT CAPACITY TUR60LENT CONTACT ABSORBER (TCA) MODULES AND
FACILITIES FOR LIMESTONE CRUSHING  AND  PREPARATION AND SLUDGE STABILIZATION.  THE BOILER FLUE GAS
FIRST PASSES THROUGH  THE ESP FOR PARTICULATE  REMOVAL AND IS THEN BOOSTED THROUGH THE TWO TCA MODULES
BY FORCED-DRAFT BOOSTER FANS.   EACH  TCA MODULE  CONTAINS A  PRESATURATOR SECTION AND TWO LEVELS OF
TURdELENT PACKING  (1.25-INCH DIAMETER  MODULE  SPHERES) WHERE THE 302 IN THE SATURATED GAS STREAM IS
REMOVED WHEN IT CONTACTS WITH  THE  LIMESTONE SLURRY.  EACH  MODULE IS EQUIPPED WITH A SEPARATE REClK-
CULATION TANK, WHERE  REACTIONS  ARE COMPLETED, FxESH SCRUBBING SLURRY IS ADDED, AND FLOE GAS CLEANING
WASTES ARE DISCHARGED.  THE CLEANED, SATURATED  FLUE GAS THEN PASSES THROUGH A SET OF MISjT ELIMINAT-
ORS  BEFORE  IT  IS  DISCHARGED TO  THE ATMOSPHERE THROUGH THE  MAIN STACK.  THE FLUE GAS CLEANING BASTES
ARE  DISCHARGED FROM  THE RtCIRCULATION  TANKS TO  A THICKENER, WHERE SOLIDS ARE SEPARATED UUT AND THE
CLARIFIED LIQUOR  is  RETURNED TO THE  PROCESS.   THE SLUDGE is FIXATED TO A CEMENTITIOUS MATERIAL (7o
TO 75 PERCENT  SOLIDS),  THEN HAULED AWAY BY FRONT-END LOADERS TO A 10-ACRE VALLEY LANDFILL AREA ON
SITE.  MAKEUP  WATER  FOR THE FGD SYSTEM IS  SUPPLIED BY COOLING TOWER BLOWOOWN WATER.  ONE UR BOTH  FGD
MODULES  CAN  BE BYPASSED DURING  EMERGENCY OF MALFUNCTION PERIODS BY THE USE OF SEAL-AIR GAS CLAMPERS.

MNITIAL OPERATING  EXPERIENCE*

      INSTALLATION OF  THE LIMESTONE FGO SYSTEM WAS COMPLETED DURING THE FIRST UUARTER OF 1977 (BEHIND
 SCHEDULE, PRIMARILY  BECAUSE OF  DELAYS  IN ELECTRICAL WORK).  FOLLOWING AIR/KATER TESTS AND CHECKOUT
 OF LIMETSONE PREPARATION FACILITIES, THE FGD  PLANT WAS STARTED UP IN EARLY APRIL 1977 FOR MECHANICAL
 SHAKEDOWN AND  DEBUGGING, WHICH  CONTINUED THROUGHOUT  THE SUMMER.  COMPLIANCE TESTING AND CERTIFICA-
 TION OF  COMMERCIAL  AVAILABILITY WERE SUCCESSFULLY COMPLETED IN SEPTEMBER, JUST BEFORE A SCHEDULED 3-
 MONTH FALL  SHUTDOWN.   TO DATE,  OPERATION OF THE SYSTEM HAS BEEN HAMPERED BY A NOMSER OF PROBLEMS!
 MIST ELIMINATOR  PLUGGING  (PIPING  TO MIST ELIMINATOR  SPRAY SYSTEM HAS BEEN MODIFICATION), CORROSION
 IN THE PRESATURATOR  (WAS RELINEO  WITH PRECRETE), CORROSION OF THE INLET/OUTLET GAS DAMPERS (REPLAC-
 ED WITH  316  SS DAMPERS),  AND FAILURE OF PRECRETE LINING IN THE SCRUBBER AND CEILCOTE IN THE STACK
 (BOTH FAILURES  IDENTIFIED  AS  APPLICATION PROBLEMS).  IN ADDITION TO THESE PROBLEMS, THE UTILITY ALSO
 FOUND IT  NECESSARY  TO CHANGE  THt  SYSTEM'S  PH  CONTROL POINT FROM 5.9 TO 5.b TO INCREASE LIMESTONE
 UTILIZATION  AND  DECREASE PLUGGING  WITHIN THE  SYSTEM.  AT PRESENT THE UTILITY IS KEEPING ONE TCA IN
 SERVICE  AND  IMPLEMENTING MODIFICATIONS ON  IT, WHICH, IF SUCCESSFUL, WILL THEN BE INCORPORATED INTO
 THE  SECOND  MODULE.
                                                   131

-------
SPRINGFIELD CITY UTILITIES                                       SOUTHWEST  UNIT  NO.  1

                                   FGD SYSTEM PERFORMANCE HISTORY

PERIOD                                        COMMENTS
AUG. 77
SEP. 77
       DURING THE REPORT PERIOD THE FGD SYSTEM WAS OPERATING ROUGHLY 60 PERCENT  OF  THE  TIME.   A NEW
       SOURCE PERFORMANCE TEST WAS RUN DURING THE SECOND WEEK OF SEPTEMBER.   LATER.  THE  UNIT  WAS
       SHUT DOWN FOR THE FIRST TURBINE INSPECTION.

OCT. 77
       DURING THE OCTOBER OUTAGE THE SCRUBBER OUTLET DAMPER HAS  MODIFIED,  SCRUBBER  PACKING  AND
       SCRUBBER OUTLET DUCTWORK LINING WERE REPLACED, AND INSULATION WAS  INSTALLED  AROUND  THE SEAL-
       AIR FAN BETWEEN THE INLET DAMPERS.  THE UNIT WAS EXPECTED TO BE BACK  IN  SERVICE  IN  DECEMBER.

NOV. 77
       PLANT WAS SHUT DOWN DURING OCTOBER AND NOVEMBER AND SCHEDULED 10 START UP  AGAIN  IN  JANUARY
       1978.  THE FOLLOWING MODIFICATIONS WERE MADE DURING THIS  PERIOD:
       * OUTLET DAMPERS WERE REPLACED BY 316 L SS DAMPERS.
       * PRESATURATOR WAS RtLINEO WITH HI-MO STEEL.
       * OUTLET DUCT WAS RELINEO WITH CEILCOTE.
       * HOLLOW PACKING BALLS WERE REPLACED BY SOLID 1.25-IN. DIAMETER BALLS.
       * LEAKING AROUND OUTLET DAMPERS WAS MINIMIZED BY SEAL-AIR FANS.

DEC. 77
JAN. 78
       THE PLANT SHUT DOWN CONTINUED UNTIL JANUARY 28 WHEN THE BOILER RESTARTED.  THE FGD  SYSTEM
       WILL BE PUT ON LINE IN FEBRUARY 1976.  DURING THE OUTAGE  ALL REMAINING MODIFICATIONS TO  THE
       FGO SYSTEM WERE COMPLETED.
       NOTE:
            THE HOLLOW PACKING BALLS WERE REPLACED WITH HEAVIER-WALL BALLS RATHER THAN  THE SOLID
            1.25 INCH DIAMETER BALLS REPORTED EARLIER.
                                                 132

-------
                  TABLE 3
PERFORMANCE DESCRIPTION FOR OPERATIONAL  FGD  SYSTEMS THROUGH  01/78



 UTILITY NAME          TENNESSEE  VALLEY  AUTHORITY

 UNIT NAME             SHAWNEE  N0.10A

 UNIT LOCATION         PADUCAH  KENTUCKY

 UNIT RATING              10 MW

 FUEL CHARACTERISTICS  COAL ^,<) PERCENT  SULFUR

 FGO VENDOR            UNIVERSAL  OIL PRODUCTS

 PROCESS               LIME/LIMESTONE  SCRUBBING

 NEK OR RETROFIT       RETROFIT

 START UP DATE          4/72

 FGD STATUS            OPERATIONAL

 EFFICIENCY,
  PARTICULATES         EXPERIMENTALLY  CONTROLLED


  302                  EXPERIMENTALLY  CONTROLLED


 WATER MAKE UP         EXPERIMENTALLY  CONTROLLED


 SLUDGE DISPOSAL       EXPERIMENTALLY  CONTROLLED


 UNIT COST


 OPERATIONAL           REFER  TO BACKGROUND INFORMATION SECTION IN TABLE  3  OF  THIS  REPORT. THIS
  EXPERIENCE           TURBULENT  CONTACT ABSORBER(TCA) LIME/LIMESTONE  SCRUBBING  SYSTEM  HAS BEEN
                       OPERATIONAL  SINCE APRIL 1972.  THIS TEST PROGRAM IS  FUNDED BY  THE  EPA.
                       TVA  IS THE CONSTRUCTOR AND FACILITY OPERATOR.  THE BECHTEL CORP.  OF SAN
                       FRANCISCO  IS THE  MAJOR CONTRACTOR, TEST DIRECTOR, AND  REPORT  WRITER.
                       DURING THE REPORT PERIOD, OPERATIONS WERE  CONDUCTED WITH  LIMESTONE
                       SLURRY CIRCULATING THROUGH THE UNIT. FORCED OXIDATION  ON  FLY  ASH-LADEN
                       FLUE GAS WAS EVALUATED.
                                               133

-------
                  TABLE 3
PERFORMANCE DESCRIPTION FOR OPERATIONAL FGD SYSTEMS  THROUGH   01/78
 UTILITY NAME          TENNESSEE VALLEY AUTHORITY

 UNIT NAME             SHAWNEE N0.10B

 UNIT LOCATION         PAOUCAH KENTUCKY

 UNIT RATING             10 MW

 FUEL CHARACTERISTICS  COAL 2.9 PERCENT SULFUR

 FGO VENDOR            CHEMICO

 PROCESS               LIME/LIMESTONE SCRUBBING

 NEW OR RETROFIT       RETROFIT

 START UP DATE           «/72

 FGD STATUS            OPERATIONAL

 EFFICIENCY,
  PARTICULATES         EXPERIMENTALLY CONTROLLED


  302                  EXPERIMENTALLY CONTROLLED


 WATER MAKE  UP         EXPERIMENTALLY CONTROLLED


 SLUDGE DISPOSAL       EXPERIMENTALLY CONTROLLED


 UNIT COST


 OPERATIONAL           REFER  TO BACKGROUND  INFORMATION  SECTION  IN  TABLE  3  OF  THIS  REPORT.  THIS
  EXPERIENCE           VENTURI/SPRAY  TOWER  LIME/LIMESTONE  SCRUBBING  SYSTEM HAS  BEEN  OPERATIONAL
                       SINCE  APRIL  1972.  THIS  TEST  PROGRAM IS FUNDED  BY  THE EPA.  TVA IS  THE
                       CONSTRUCTOR  AND  FACILITY OPERATOR.  THE BECHTEL CORP. OF  SAN FRANCISCO  IS
                       THE  MAJOR CONTRACTOR,  TEST DIRECTOR,  AND  REPORT WRITER.  DURING THE  REPORT
                       PERIOD, FORCED OXIDATION WAS  EVALUATED ON FLY  ASH-FREE FLUE GAS WITH
                       LIME SLURRY  AS THE SCRUBBING  AGENT.
                                               134

-------
                                       BACKGROUND  INFORMATION
                                                  ON
                                       SHAWNEE  NOS. 10A AND 108

     IN  JUNE  1968,  THE EPA INITIATED  A PROGRAM  TO  TEST  PROTOTYPE LIME AND LIMESTONE SYSTEMS  FOR
REMOVAL  OF  SULFUR DIOXIDE AND PARTICULATE  FROM  COAL-FIRED BOILER FLUE EASES   THE PROGRAM WAS
CARRIED  OUT IN A TEST FACILITY INCORPORATED  INTO  THE  FLUE GAS DUCTWORK OF UNIT NO. 10,  A  COAL-FIRED
BOILER  AT  THE TVA SHAWNEE POWER STATION, PAOUCAM,  KENTUCKY.  TVA IS THE CONSTRUCTOR AND FACILITY
OPERATOR AND  BECHTEL CORP. IS THE MAJOR  CONTRACTOR, TEST DIRECTOR,  AND REPORT WRITER.

     THE TEST FACILITY CONSISTS OF  THREE PARALLEL  SCRUBBER SYSTEMS  OF PROTOTYPE SIZE,  TREATING  PART
OF THE  FLUE GAS FROM THE BOILER.  EACH SCRUBBER TRAIN IS CAPABLE OF TREATING APPROXIMATELY JO,000
ACFM OR THE EQUIVALENT OF APPROXIMATELY  10 MW  OF  POWER  PLANT GENERATING CAPACITY.

     THREE PARALLEL WET SCRUBBER  SYSTEMS WERE  SELECTED  FOR THE TEST PROJECT:  1)  A VENTURI WITH  A
SPRAY TOWER AFTER ABSORBER, 2) A  TURBULENT CONTACT ABSORBER (TCA),  AND 3) A MARBLE-BEO  ABSORBER.
THE VENTURI SYSTEM, MANUFACTURED  BY  CHEMICAL CONSTRUCTION CO., CONTAINS AN ADJUSTABLE  THROA1  IHAT
PERMITS CONTROL AND VARIATION UF  PRESSURE  DROP  UNDER  A  WIDE RANGE OF FLOW CONDITIONS.   THE TCA  UNIT,
MANUFACTURED BY UNIVERSAL OIL PRODUCTS,  INCORPORATES  A  FLUIDIZED BED OF LOW DENSITY PLASTIC  SPHERES
THAT ARE FREE TO MOVE BETWEEN RETAINING  GRIDS.   THE MARBLE-BED ABSORBER, SUPPLIED BY COMBUSTION
ENGINEERING CO., USES A PACKING OF  3/4-INCH  GLASS MARBLE SPHERES AND A TURBULENT  LAYER  UF LIQUID  AND
GAS ABOVE THE MARBLE LAYER TO ENHANCE MASS TRANSFER.

     IN JUNE  1974, THE EPA BEGAN  A  3-YEAR  ADVANCED TEST PROGRAM AT  THE SHAWNEE FACILITY WITH THESE
MAJOR GOALS:  ti) CONTINUATION OF LONG-TERM  TESTING,  WITH EMPHASIS  PLACED UPON THE RELIABLE  OPERAT-
ION OF MIST ELIMINATION SYSTEMS AT  INCREASED GAS  VELOCITY, (2) INVESTIGATION OF ADVANCED  PROCESS  AND
EQUIPMENT DESIGN VARIATIONS FOR IMPROVING  SYSTEM  RELIABILITY AND PROCESS ECONOMICS, AND C3)  LONG-
TERM RELIABILITY TESTING ON PROMISING PROCESS  AND EQUIPMENT DESIGN  VARIATIONS.

     THE TWO  PARALLEL SCRUBBING SYSTEMS  OPERATING DURING THE ADVANCED PROGRAM ARE THE  VENTURI/SPRAY
TOWER SYSTEM  AND THE  TCA UNIT.  GENERAL  PROCESS FLOW  DIAGRAMS OF THE TWO PROTOTYPE UNITS  ARE PROVID-
ED  IN APPENDIX  B.  OPERATION  UF THE MARBLE-BED  ABSORBER UNIT HAS BEEN PERMANENTLY DISCONTINUED.
     EACH  OF  THE SCRUBBING SYSTEMS  CONTAINS  ITS OWN SLURRY HANDLING FACILITIES AND CAN  TREAT APPROX-
IMATELY 30,000  ACFM  OF GAS AT 300 F CONTAINING  1800 TO  1000 PPM OF  SULFUR DIOXIDE AND  2 TO <4
GRAINS/SCF OF PARTICULATE.  BOILER  NO.  1  NORMALLY BURNS A HIGH-SULFUR BITUMINOUS  CUAL.

     FROM  JUNE  1974  TO JANUARY  1976,  MIST  ELIMINATION AND LIMESTONE UTILIZATION TESTS  WERE CONDUCTED
AT  THE  SHAWNEE  FACILITY.   DURING  THIS TEST PERIOD THE VENTURI/SPRAY TOWER SYSTEM  WAS OPERATED  ON
BOTH LIME  AND LIMESTONE AND THE TCA SYSTEM WITH LIMESTONE.  TESTING WAS PERFORMED UNDER A CLOSED-
WATER OPERATION MODE.  DURING  THIS  PERIOD  THE SLURRY  SOLIDS CONTAINED APPROXIMATELY 40  TO 50
PERCENT-BY-WEIGHT  FLY ASH  BECAUSE OF RELATIVELY HIGH GAS INLET PARTICULATE LOADING.  THIS TESTING
PROGRAM IS SCHEDULED  TO RUN THROUGH TO FEB.  1978.

     ADDITIONAL INFORMATION AND DATA CONCERNING THE DETAILS OF THE  ADVANCED TEST  PROGRAM  ARE PRESEN-
 TED IN  THE PERFORMANCE TABLE  THAT FOLLOWS.
                                                   135

-------
TENNESSEE VALLEY AUTHORITY                                              SHAWNEE  UNIT NOS. 10A AND 10B

SEP. 75     THIS EXPERIMENTAL EPA-FUNDED OPERATION  IS PROCEEDING  WITH  THE  TEST  PROGRAM.  TWO
OCT. 75     AbSORBER MODULES ARE CURRENTLY OPERATIONAL  (10  MW  EACH).  THE MAKBLE-BED ABSORBER IS
            STILL INOPERATIVE (SINCE JULY  1973).  CURRENT EXPERIMENTS  ARE  RELATED  TO MIST ELlMINATQK
            SECTION.

NOV. 75     RECENT TESTING AT SHAWNEE HAS  SHOWN THAT THE CHEVRON  MIST  ELIMINATORS  IN BOTH THE SPRAY
DEC. 75     TOWER AND THE TCA CAN HE KEPT  FREE OF SOLIDS BUILDUP  AT  HIGH ALKALI  UTILIZATION (GREATER
            THAN 90 PERCENT), USING ONLY INTERMITTENT WASHING  WITH  AVAILABLE  RAW WATER.  THIS HIGH
            UTILIZATION IS NORMALLY ACHIEVED WITH LIME. IT  HAS BEEN  ACHIEVED  WITH  LIMESTONE AT RED-
            UCED SCRUBBER INLET SLURRY PH  (ABOUT 5.2) AND WITH THREE EFFLUENT TANKS IN SERIES TO
            SIMULATE A PLUG-FLOW REATOR.   TESTING   IS CONTINUING  TO  DETERMINE THE  EFFECTS OF PROCESS
            VARIABLES UN MIST ELIMINATOR PERFORMANCE AND ON LIMESTONE  UTILISATION.   FUTURE PLANS
            INCLUDE:  (1) FACTORIAL TESTING WITH LIME AND LIMESTONE  TO DETERMINE THE EFFECTS OF
            PROCESS VARIABLES ON S02 REMOVAL AND (2) TESTING THE  OXIDATION  UF SLUDGE TO GYPSUM IN
            THE VENTURI/SPRAY TOWER SYSTEM USING AIR SPARGING  OF  AN  ACIDIFIED SLURRY BLEED STREAM.

JAN. 76     THE ADVANCED TEST PROGRAM IS CONTINUING.  HIGHLIGHTS  OF  THE PROGRAM  ARE AS FOLLOWS:
FEB. 76     EVALUATE SCRUBBER OPERAblLITY  DURING VARIABLE LOAD OPERATION.
            CONTINUE LONG-TERM RELIABILITY TESTING.
            INVESTIGATE METHODS FOR IMPROVING WASTE SOLIDS  SEPERATION.
            CONTINUE SLUDGE OXIDATION AND  SLUDGE FIXATION STUDY PROGRAMS.
            EVALUATE SYSTEM PERFORMANCE AT REDUCED  FLY  ASH  LOADINGS.
            DETERMINE THE PRACTICAL UPPER  LIMITS OF S02 REMOVAL EFFICIENCY.
            EVALUATE ADDITION OF MAGNESIUM ION TO THE SCRUBBING SLURRY.
            CHARACTERIZE ALL STACK GAS EMISSION COMPONENTS.
            EVALUATE MATERIALS OF CONSTRUCTION OF ALL SCRUBBER AND  PLANT-RELATED COMPONENTS.
            DEVELOP A COMPUTER PROGRAM FOR DESIGN AND COST  ANALYSIS  OF FULL-SCALE  LIME/LIMESTONE
            SYSTEM.

MAR. 76     BECHTEL REPORTED THAT THE FACTORIAL TEST PROGRAM,  EVALUATING THE  PERFORMANCE OF THE
            LIME/LIMESTONE SCRUBBING

APR. 76     SYSTEMS WITH AND WITHOUT MAGNESIUM ADDITION HAS BEEN  COMPLETED.   CURRENTLY TESTING  IS
            PROCEEDING ON THE EVALUATION OF SYSTEM  PERFORMANCE AS A  FUNCTION  OF  LOW RESIDENCE  TIMES
            (1.5 TO 5.0 MINUTES) IN THE RECYCLE TANKS.  IN  ADDITION, A FLY-ASH-FREE DUCT IS BEING
            INSTALLED AT THE TEST FACILITY, THUS ENABLING EVALUATION OF SYSTEM  PERFORMANCE IN  THE
            ABSENCE OF FLY ASH.

MAY  7fa      THE TEST DIRECTOR, BECHTEL, PROVIDED THE FOLLOWING INPUT CONCERNING  THE OPERATION  OF
            THE EXPERIMENTAL SCRUBBING SYSTEMS DURING THE REPORT  PERIOD.

JUN. 76     THE EFFECT OF MGO ADDITION WAS EXPLORED IN  BOTH SCRUBBER SYSTEMS.  RESULTS INDICATE MAG-
            NESIUM  ION IN THE SCRUBBER SLURRY LIQUOR ENHANCES  303 REMOVAL  AND CAN  DEPRESS SULFATE
            SUPERSATURATION.  IT WAS FOUND THAT THE MAGNESIUM  ION CONCENTRATION  HAD TO EXCEED  THE
            EQUIVALENT CHLORIDE ION CONCENTRATION TO HAVE AN EFFECT  ON S02  REMOVAL.
            IN  THE  TCA UNIT, WITH LIMESTONE SLUkRY, S02 REMOVAL WAS  INCREASED FROM  75  TO 95 PERCENT
            BY  INCREASING THE MAGNESIUM ION CONCENTRATION TO 9,000  PPM IN  EXCESS OF EQUIVALENT
            EQUAL  TO 6 PERCENT BY WEIGHT OF THE LIMESTONE ADDITION  RATE.   IN  THE VENTURI/SPRAY
            TOWER  SYSTEM, WITH LIME SLURRY, 302 REMOVAL WAS INCREASED  FROM  75 TO 90 PERCENT BY  IN-
            CREASING MAGNESIUM ION CONCENTRATION TO 2,000 PPM  IN  EXCESS OF  EQUIVALENT  CHLORIDE  ION.
            THE MAGNESIUM OXIDE ADDITION RATE WAS 2 PERCENT BY WEIGHT  OF THE  LIME  ADDITION RATE.
            BOTH SCRUBBING SYSTEMS OPERATED IN THE  SUBSATURATED SULFATE MODE  WHEN  MAGNESIUM OXIDE
            WAS ADDED.   INLET so2 CONCENTRATIONS DURING THE TESTS AVERAGE  APPROXIMATELY 3,000  PPM
            DURING  THESE TESTS.
            FOLLOWING THE TEST BLOCKS MENTIONED ABOVE,  BOTH SCRUBBERS  ARE  OPERATING WITH LIME  SLURRY
            SCRUBBING SOLUTIONS, THE TCA SYSTEM ON  FLUE GAS CONTAINING FLY  ASH  AND  THE VENTURI/SPRAY
            TOWER  SYSTEM ON FLY ASH-FREE FLUE GAS.

JUL. 76     EXPERIMENTAL OPERATION OF THE  EPA/TVA ALKALI SCRUBBING  TEST FACILITY CONTINUED DURING
            THE REPORT PERIOD.  BECHTEL,THE TEST DIRECTOR,  PROVIDED  THE FOLLOWING  INPUT CONCERNING
AUG. 76     THE OPERATION OF THE PROTOTYPE TEST UNITS.
            VENTUHI/SPRAY TOWER SYSTEM:  THIS SYSTEM RAN ON FLY ASH-FREE FLUE GAS  USING A LIME
            SLURRY  SCRUBBING SOLUTION.  NO SIGNIFICANT  DIFFERENCES  IN  soa  REMOVAL,  GYPSUM SATURATION
            AND SULFITE OXIDATION WERE DETECTED (VERSUS FLY ASH-LADEN  FLUE  GAS).  ONE  DIFFERENCE
            NOTED  WAS THE FILTER CAKE SOLIDS CONTENT WHICH  WAS APPROXIMATELY  10  PERCENT LOWER  FOR
            THE FLY ASH-FREE SLUDGE (40 TO 50 PERCENT SOLIDS)  VERSUS  THE FLY  ASH-LADEN SLUDGE  (50 TO
            60  PERCENT SOLIDS).  IN ADDITION, OPERATION IN  A LOW  RESIDENCE  TIME  MODE (3 MINUTES) WAS
            EXPLORED. SCALE-FREE OPERATION WAS ACHIEVED IN  THIS MODE  UNDER  THE  FOLLOWING CONDITIONS:
            » PERCENT SOLIDS (NO FLY ASH)  IN THE RECIRCULATED  SLURRY,  Pri UF  THE  SCRUBBER LIQUID
            INLET  WAS 6.0, SUPERFICIAL GAS VELOCITY OF  9.«  FT./SEC.,  AND A  TOTAL LIUUID-TO-GAS RATIO
            (L-G)  OF 71 GAL./MCF.  SOME SCALE FORMATION OCCURED WHEN  THE SOLIDS  CONTENT IN THE  RE-
            CIRCULATED SLURRY DROPPED BELOW THE a PERCENT LEVEL.
            TCA SYSTEM:  THIS SYSTEM OPERATED ON FLY ASH-LADEN FLUE  GAS USING A  LIME SLURRY SCRUBB-
            ING SOLUTION INNOCULATED WITH  MAGNESIUM OXIOE.  GYPSUM  SU8SATURATION OPERATION WAS ACHI-
            EVED UNDER THE FOLLOWING CONDITIONS:  MAGNESIUM ION CONCENTRATION EXCEEDED THE
            CHLORIDE ION CONCENTRATION BY  2000 PPM, SUPERFICIAL GAS  VELOCITY  WAS 12.5 FT./SEC.r L/G
                                                   136

-------
TENNESSEE  VALLEY AUTHORITY                                        SHArtNEE  UNJT  ^  m  ^  ^

          WAS 50.   THE SCRUBBING SOLUTION  INLET  PH  WAS  7.0,  AND  RESIDENCE TIME  WAS  4-MINUTFs   THC
          802 REMOVAL EFFICIENCY WAS APPROXIMATELY  90  PERCENT.   WHEN L/G  WAS  REDUCED  ?o  «  IMI.P
          ALL OTHER CONDITIONS HEMAINED CONSTANT, SEVERE  GYPSUM  SCALE FORMATION RESULTED    rT
          CREASING THE EFFECTIVE MAGNESIUM  ION CONCENTRATION TO  «000 PPM  AND  THE IcftUB^R .  SMTP
          INLET PH TO 8.0 DID NOT AMELIORATE  THE SCALE  PROBLEM.   PRESENTLY,  THE VEN?UKSR

          '
                                                                            THE
                                                         "*
SEP.  76    IN  SEPTEMBER AND OCTOBER 1976, THE VENTURI/SPRAY  SYSTEM WAS  OPERATED WITH FLY ASH-FREE
OCT.  76    FLUE  GAS  USING LIME SLURRY WITH ADDED MAGNESIUM OXIDE.  TYPICAL TEST CONDITIONS WERE 9 a
          FT/SEC  SPRAY TOWER GAS VELOCITY, 21 GAL/MCF VENTURI L/G,  50  GAL/MCF SPRAY TOWER L/G, 8
          PERCENT SLURRY SOLIDS (FLY ASH-FREE), 3 MINUTES RESIDENCE  TIME, 7.0 SCRUBBER INLET PH,
          AND £000  PPM EFFECTIVE MG ION CONCENTRATION (I.E., EXCESS  OVER EQUIVALENT CHLORIDE ION)
          RESULTS WERE NOT CONSISTENT AT THESE CONDITIONS.  DURING  ONE PERIOD, SCRUBBING INLET
          LIQUOR  GYPSUM SATURATION AVERAGED 65 PERCENT WITH 80 PERCENT S02 REMOVAL AND WITH SOME
          GYPSUM  SCALE FORMATION. IN A LATER PERIOD, AT SEEMINGLY IDENTICAL TEST CONDITIONS, GYP-
          SUM SATURATIONS DROPPED TO 10 PERCENT WITH 98 PERCENT 302  REMOVAL AND THE SCRUBBER DE-
          SCALED.  A SEVEN-WEEK PROGRAM OF INTENSIVE FLUE GAS CHARACTERIZATION TESTING wAS STARTED
          IN  MID-OCTOBER ON THE VENTURI/SPRAY TOWER SYSTEM.  THESE  TESTS ARE BEING MADE TO MEASURE
          SIMULTANEOUS INLET AND OUTLET FLUE GAS PARTICULATE MASS LOADING, PARTICULATE SIZE DIS-
          TRIBUTION, AND GASEOUS S03 CONCENTRATION.  THE TCA SYSTEM  CONTINUED TO OPERATE DURING
          THIS  PERIOD ON FLY ASH-LADEN FLUE GAS USING LIME  SLURRY WITH ADDED MAGNESIUM OXIDE.  THE
          TEST  RESULTS SOFAR INDICATED THAT THE DEGREE OF SULFATE (GYPSUM) SUBSATURAT ION IS A SEN-
          SITIVE  FUNCTION OF THE EFFLUENT RESIDENCE TIME CONDITIONS: GAS VELOCITY 12.5 FT/SEC, L/G
          OF  50,  PH OF 7.0, 8000 PPM OF MG ION, AND 8 PERCENT SULIDS.  AT THESE CONDITIONS GYPSUM
          SATURATIONS WERE 95, 50, AND 92 PERCENT, AT RESIDENCE TIMES  OF 3, H, AND 12 MINUTES,
          RESPECTIVELY.  FURTHER TESTS WERE RUN AT 37 GAL/MCF L/G,  AND 8.0 SCRUBBER INLET PH WITH
          OTHER CONDITIONS THE SAME.  DURING THESE TESTS GYPSUM SATURATIONS WERE 95, 95, 50, AND
          90  PERCENT AT 3, 4, 5.4, AND 16 MINUTES RESIDENCE TIMES, RESPECTIVELY.

NOV. 76    FROM MID-OCTOBER THROUGH EARLY DECEMBER AN INTENSIVE FLUE  GAS CHARACTERIZATION TESTING
DEC. 76    PROGRAM WAS CONDUCTED ON THE VENTURI/SPRAY TOWER  SYSTEM WITH LIME SLURRY.
          OVER THE RANGE TESTED, OUTLET PARTICULATE MASS LOADING WAS FOUND TO BE INDEPENDENT OF
          SLURRY  COMPOSITION (8 TO 15 PERCENT SUSPENDED SOLIDS, 3,000  TO 16,000 PPM DISSOLVED
          SOLIDS),  GAS FLOW RATE (20,000 TO 35,000 ACFM) , SPRAY TOWER  LIQUID RATE (0 TO 1,400 GPM)
          AND VENTURI PRESSURE DROP (3 TO 9 INCHES H20) .  WITH 4 TO  6  GR/DSCF PARTICULATE IN THE
          INLET,  TYPICAL OUTLET LOADINGS WERE 0.02 TO 0.04  GR/DSCF.  WHEN OPERATING WITH FLUE GAS
          FROM THE ELECTROSTATIC PRECIPITATOR (0.1 TO 0.4 GR/DSCF TO THE SCRUBBER), THE SCRUBBER
          OUTLET  LOADING AVERAGED 0.005 GR/OSCF.  THUS, ENTRAINED SLURRY FROM THE MIST ELIMINATOR
          MUST HAVE BEEN LESS THAN 0.005 GR/DSCF.  SIZE DISTRIBUTION DATA ARE STILL BEING ANALYZ-
          ED.  SULFURIC ACID MIST VALUES WERE APPROXIMATELY 2 TO 25  PPM AT THE SCRUBBER INLET AND
          REMOVALS HAVE BEEN ABOUT 50 TO 75 PERCENT.
          FOR THE REMAINDER OF DECEMBER THE VENTURI/SPRAY TOWER SYSTEM WAS DOWN FOR MODIFICATIONS
          FOR TWO-STAGE OXIDATION TESTING.  SEE APPENDIX B  FOR A PROCESS FLOW DIAGRAM.
          DURING  NOVEMBER THE TCA WAS OPERATED WITH FLY-ASH CONTAINING FLUE GAS USING LIME SLURRY
          WITHOUT ADDED MAGNESIUM OXIDE.  OPERATING CONDITIONS WERE  12.5 FT/SEC GAS VELOCITY, 50
          GAL/MCF L/G, 6.0 SCRUBBER INLET PH, AND & TO 15 PERCENT SLURRY SOLIUS.  AT THESE CONDIT-
          IONS THE S02 REMOVAL WAS ABOUT 80 PERCENT.
          FLY-ASH FREE LIMESTONE TESTS WITHUUT MAGNESIUM OXIDE ADDITION BEGAN ON THE TCA SYSTEM IN
          LATE NOVEMBER.  TYPICAL OPERATING CONDITIONS WERE 12.5 FT/SEC GAS VELOCITY, 50 GAL/MCF
          L/G,  AND 1.1 TO 1.2 STOICHIOMETRIC RATIO.  AT THE SAME STOICHIOME1 R Y , THE PH OF THE FLY-
          ASH FREE SLURRY WAS 0.2 TO 0.3 UNITS HIGHER THAN  OBSERVED  IN PREVIOUS RUNS WITH FLY ASH.

JAN. 77    THE VENTURI/SPRAY TOWER SYSTEM HAS BEEN OPERATED  IN A TwO-SER IES-SCRUBBER MODE WITH FORCED
FEB. 77    OXIDATION SINCE EARLY JANUARY 1977 AF1ER SYSTEM MODIFICATIONS TO ALLOW OPERATION OF THE
          VENTURI AND SPRAY TOWER WITH INDEPENDENT SLURRY RECIRCULA T ION LOOPS.  SULFITE OXIDATION
          WAS CARRIED OUT IN AN 8 FT. DIAMETER VENTURI (PRE-SCRU6BER)  EFFLUENT HOLD TANK WHICH HAD A
          130 - 1/8 INCH HOLE AIR SPARGER IMMERSED IN 18 FT. UF SLURRY.  THt SPRAY TOWER (AFTER
          SCRUBBER) FUNCTIONED AS A PRIMARY S02 ABSORBER.
          TYPICAL OPERATING CONDITIONS, USING LIMESTONE SLURRY, WERE 6.7 FT/SEC SPRAY TOWER GAS
          VELOCITY, 20-30 GAL/MCF VENTURI L/G, 70 GAL/MCF SPRAY TOWER  L/G, 15 PERCENT SOLIDS (WITH
          FLY ASH)  IN VENTURI RECIRCULATED SLURKY, 4.5-5.0  VENTURI  INLET (OXIDATION TANK) PH, AND
          11.3 MINUTES OXIDATION TANK RESIDENCE TIME (BASED ON 600  GPM SLURRY FLOW TO VENTURI).
          DURING  THESE TESTS, AVERAGE OVERALL SULFITE OXIDATION RANGED FROM 93 TO 99 PERCENT AT AIR
          STOICHIOMETRIC RATIO OF 1.0 TO 4.7 LB-ATOMS OXYGEN/LB-MULE S02 ABSORBED.  CORRESPONDING
          AVERAGE OXIDATION IN THE SPRAY TOWER RANGED FROM  10 TO 16  PERCENT.  AVERAGE OVERALL LIME-
          STONE UTILIZATION RANGED FROM 83 TO 96 PERCENT.   NO SCALING  WAS EXPERIENCED IN EITHER
          SCRUBBER.  AVERAGE FILTER CAKE SOLIDS WERE 79 TO  86 PERCENT  BY WEIGHT COMPARED WITH 55-65
          PERCENT WITHOUT FORCED OXIDATION.  SLURRY SOLIDS  SETTLING  RATE RANGED 0.5 TO 1.4 CM/MIN, 5
          TO  10 TIMES FASTER THAN THAT FOR UNOXIOIZED SLURRY.  FINAL SETTLED DENSITY RANGED 65-80
          PERCENT SOLIDS COMPARED WITH 45-60 PERCENT FOR SLURRY WITHOUT FORCED OXIDATION.
          FLY ASH-FREE LIMESTONE TESTING ON THE TCA SYSTEM  WAS COMPLETED IN EARLY FEBRUARY.  THE  PH
          OF  THE  FLY ASH-FREE SLURRY WAS 0.2 TO 0.3 UNITS HIGHER THAN  OBSERVED IN PREVIOUS RUNS WITH
          FLY ASH.   IN ADDITION, THE FLY ASH-FREE SLURRY APPRtARED  TO  HAVE INFERIOR SOLIDS DE-
          WATERING CHARACTERISTICS.  FOR EXAMPLE, THE CENTRIFUGE CAKE  SOLIDS AVERAGED ABOUT 50
          PERCENT COMPARED WITH ABOUT 60 PERCENT FOR SLUDGE CONTAINING FLY ASH.
                                                  137

-------
TENNESSEE VALLEY AUTHORITY                                        SHAWNEE  UNIT  NOS.  10A AND JOB

          INTENSIVE FLUE SAS CHARACTERIZATION  TESTING  WITH LIMESTONE  SLURRY  ON THE  TCA SYSTEM BEGAN
          IN EARLY FEBRUARY AND ENDED  IN EARLY MARCH 1977.   PRELIMINARY ANALYSIS  OF THE DATA SHOWED
          AN OUTLET MASS LOADING OF 0.04-0.08  GRAIN/DSCF  FOR  FLUE  GAS  CONTAINING  FLY ASH AND 0.02-
          0.03 GRAINS/DSCF FOR FLUE GAS WITHDRAWN DOWNSTREAM  OF  THE ESP.   IT WAS  ESTIMATED THAT
          THESE OUTLET MASS LOADINGS CONTAINED ABOUT 0.03 GRAIN/DSCF  FLY  ASH,  0.02  GRAIN/DSCF RE-
          ENTRAINEO SLURRY SOLIDS, AND 0.015 ENTRAINED DISSOLVED  SOLIDS  (WHEN  A CONTINUOUS MIST
          ELIMINATOR UNDER WASH WAS USED).  THESE VALUES  VARY DEPENDING ON  THE MIST ELIMINATOR WASH
          SCHEME AND GAS FLOW RATE.

MAR. 77   DURING MARCH, THE VENTURI/SPRAY TOWER WAS TESTED WITH  LIME  SLURRY  AND FLY ASH LADEN FLUE
          GAS IN A TWO-STAGE SCRUBBER  MODE WITH FORCED OXIDATION.  OPERATION WITH LIME WAS SIMILAR
          TO THE PREVIOUSLY REPORTED LIMESTONE OPERATION  WITH GREATER  THAN  95  PERCENT  OXIDATION AT
          AN AIR STOICHIOMETRIC RATIO  OF 1.5 LB-ATOMS  OXYGEN/LB-MOLE  S02  ABSORBED WITH A SIMPLE AIR
          SPARGER IN A VENTURI HOLD TANK.  SLURRY SOLIDS  SETTLING  RATE VARIED  FROM  0.6 TO 1/9 CM/MIN
          (A 5 TO 10 FOLD ENHANCEMENT  OVER UNOX10IZED  SLURRY) AND  FILTER  CAKE  SOLIDS RANGED FROM 74
          TO 68 PERCENT (COMPARED WITH 45 TO 60 PERCENT WITH  UNOXIDIZED SLURRY).
          TWO MAJOR DIFFERENCES BETWEEN LIME AND LIMESTONE WERE  OBSERVED  IN  A  TWO-STAGE FORCED
          OXIDATION.  TO MAINTAIN PH CONTROL,  IT WAS NECESSARY TO  FEED LIME  TO BOTH STAGES.  WITH
          LIMESTONE, FEED ONLY TO THE  SECOND STAGE WAS ADEQUATE.   TO  MAINTAIN  80  PERCENT 802
          REMOVAL, IT WAS NECESSARY TO OPERATE WITH HIGHER SLURRY  SOLIDS  CONCENTRATION IN THE SPRAY
          TOWER LOOP WITH LIMESTONE (15 PERCENT) THAN  WITH LIME  (6 PERCENT), RESULTING IN A TIGHTER
          WATER BALANCE WITH LIMESTONE AND INADEQUATE  WATER  TO FLUSH  THE  MIST  ELIMINATOR.
          PRELIMINARY LIMESTONE TYPE AND GRIND TESTS MADE ON  THE  TCA  SYSTEM  DURING  MARCH INDICATED
          THAT 802 REMOVAL IS IMPROVED BY THE  USE OF FINER GROUND  LIMESTONE.   S02 REMOVAL WITH
          EQUIVALENT GROUND FREDONIA WHITE AND LONGVIEW,  ALABAMA  LINESTONES  WAS THE SAME.
          BLEEDSTREAM FORCED OXIDATION TESTS ARE BEING CONDUCTED  WITH  A PENBERTHY ELL-S EJECTOR IN A
          CLOSED LOOP AROUND A BLEED STREAM HOLD TANK.  INITIAL  TESTS  WERE  UNSUCCESSFUL DUE TO HIGH
          PH OF 7 TO 8 IN THE HOLD TANK.  BY LOWERING  THE HOLD TANK PH TO  5  TO 6, SULFITE OXIDATION
          UP TO 98 PERCENT WAS ACHIEVED.

APR. 77   UNIT  10 BOILER WAS SHUT DOWN FOR A SCHEDULED TWO-MONTH  MAINTAINANCE  OUTAGE.   bECAUSE OF
MAY  77    THE BOILER OUTAGE, THE SHAWNEE SCRUBBERS WILL NOT  OPERATE OURRING  APRIL AND  MAY.
JUN. 77   SCRUBBER OPERATION RESUMED ON JUNE 15 AFTER  A 10-WEEK  SCHEDULED  MAINTENANCE  OUTAGE  ON THE
          BOILER.

JUL. 77   THE VENTURI/SPRAY TOWER SYSTEM CONTINUED TO  OPERATE WITH TWO SCRUBBER STAGES AND  FORCED
          OXIDATION BY MEANS OF AN AIR SPARGING RING IN THE  VENTURI HOLD  TANK.  IN  JUNE AND JULY,
          OPERATION WAS WITH LIME SLURRY AND FLY ASH-FREE FLUE GAS.   THE  SYSTEM PERFORMED WELL WITH
          LITTLE DIFFERENCE FROM THE PREVIOUS  LIME SLURRY TEST BLOCK  WHEN  THERE WAS FLY ASH IN THE
          FLUE  GAS.  TYPICAL RESULTS WERE ABOUT 97 PERCENT SULFITE OXIDATION AT AN  AIR STOICHIOMETRY
          OF 1.6 LB-ATOMS OXYGEN/LB-MOLE S02 ABSORBED  AND AN  OXIDATION TANK  PH OF 5.5.  TYPICAL
          SOLIDS SETTLING RATE WAS ABOUT 2 CM/MIN  (AN  ORDER  OF MAGNITUDE  BETTER THAN WITH UNOXIDIZED
          SLURRY) AND FILTER CAKE SOLIDS CONCENTRATION AVERAGED  ABOUT  so  PERCENT  (COMPARED  WITH 45
          TO 60 PERCENT WITH UNOXIDIZEO SLURRY).
          THE TCA SYSTEM OPERATED WITH FORCED  OXIDATION IN THE HOLD TANK  ACHIEVED BY CIRCULATING
          SLURRY THROUGH AN AIR EOUCTOR.  IN JUNE AND  JULY,  OPERATION  WAS  WITH LIMESTONE SLURRY AND
          FLY ASH IN THE FLUE GAS.  SULFITE OXIDATION  WAS POOR IN  INITIAL  TEST  (LESS THAN 90  PER-
          CENT) MAINLY BECAUSE OF INADEQUATE AIR/SLURRY CONTACT  IN THE HOLD  TANK.   BY  INCREASING
          AGITATOR SPEED  (TO 68 RPM),  HOLD TANK SLURRY LEVEL  (TO  12FT) AND  DECREASING  PH (TO  LESS
          THAN  5.5) IN THE SLURRY TO THE EDUCTOR, SULFITE OXIDATION ABOVE  90 PERCENT HAS CONSIS-
          TANTLY ACHIEVED AT AN AIR STOICHIOMETRY OF ABOUT 4.5 LB/ATOMS OXYGEN/LB-MOLE 802  ABSORBED.
          WASTE SOLIDS PROPERTIES WERE ENHANCED WITH OXIDATION TO  ABOUT THE  SAME  EXTENT AS  OBSERVED
          IN THE VENTURI/SPRAY TOWER SYSTEM.   ADDITIONAL  TESTING  WILL  BE  DIRECTED TOWARD ACHIEVING
          90 PERCENT OR BETTER SULFITE OXIDATION AT A  REDUCED AIR  STOICHIOMETHY.

 AUG. 77   THE VENTURI/SPRAY TOWER SYSTEM CONTINUED TO  OPERATE WITH TWO SCRUBBER STAGES AND  FORCED
 SEP. 77   OXIDATION USING AN AIR SPARGER IN THE VENTURI HOLD  TANK.  OPERATION  DURING AUGUST AND
          SEPTEMBER WAS WITH LIMESTONE SLURRY  AND FLUE GAS WITH  LOW FLY ASH  LOADING (FLUE GAS FROM
          DOWNSTREAM OF THE ESP).  THE SYSTEM  PERFORMED WELL  AT  4.5 TO 5.0  OXIDATION PH,  WITH LITTLE
          DIFFERENCE FROM THE PREVIOUS LIMESTONE TESTS WHEN  THE  FLUE  GAS  HAD HIGH FLY  ASH LOADING.
          (THE  PREVIOUS TESTS WERE MADE ONLY AT OXIDATION PH  OF  4,5 AND 5.0).
          FOR THE AUGUST AND SEPTEMBER TESTS,  THE OXIDATION  PH WAS FURTHER  INCREASED TO 5.5,  AP-
          PROACHING THE PH IN THE SPRAY TOWER.  THIS CAUSED  SOME  DIFFICULTIES  IN  THE OXIDATION PH
          CONTROL AND WIDER FLUCTUATIONS IN VENTURI AND SPRAY TOWER LIMESTONE  STOICHIOMETRIC  RATIUS.
          HOWEVER, NEAR COMPLETE OXIDATION WAS STILL ACHIEVED AT  THE  HIGHER  PH.   TYPICAL RESULTS
          WERE  BETTER THAN 97 PERCENT  SULFITE  OXIDATION AT AN AIR  STOICHIOMETKY OF  1.7 ATOMS  OXYGEN/
          MOLE  S02 ABSORBED AND AN OXIDATION PH OF 5.5.   THE  FILTER CAKE  SOLIDS CONTENT AVERAGED
          BETTER THAN 85 PERCENT.  TESTS WERE  ALSO CONDUCTED  WITHOUT  THE  DESUPERSATUHATION TANK IN
          THE VENTURI SLURRY LOOP AND  WITH THE OXIDATION  TANK LEVEL DROPPED  FHOM  18 TO 14 FT  rtlTHOUT
          ADVERSE EFFECTS.
          DURING AUGUST AND SEPTEMBER, THE TCA SYSTEM  WAS OPERATED MOSTLY  IN A TWO-TANK FORCED
          OXIDATION MODE USING AN AIR  EDUCTOR.  THE TCA EFFLUENT  (LIMESTONE  SLURRY  WITH HIGH FLY ASH
          LOADING) WAS COLLECTED IN A  SMALL LOW-PH SLURRY HOLD TANK AND THEN PUMPED THROUGH THE AIR
          EOUCTOR TO THE REGULAR HOLD  TANK WHERE LIMESTONE WAS ADDED,  THUS TAKING THE  ADVANTAGE OF
          THE LOW PH SLURRY THROUGH THE AIR EOUCTOR FOR IMPROVED  SULFITE  OXIDATION  AND HIGH PH
          SLURRY TO TCA FOR BETTER S02 REMOVAL.
                                                  133

-------
TENNESSEE  VALLEY AUTHORITY                                        CLJ,,ir,
                                                                  SHAWNEfc  UNIT  NUS.  10A  AND  lllb

          TESTS WERE MADE BOTH WITH  THE  AIR  EDUCTOR MOUNTED ON TOP OF THE FFFlilFNT  urn n  T K
          DOWNWARD SLURRY DISCHARGE,  AND WITH THE EDUCTUR MOUNTED oS'sol OF  T"HF  TANK w, i   /  "
          DISCHARGE TO THE BOTTOM  OF  THE TANK.   AVERAGE SULFITE OXIDATION RANGED  J£nM » in*^'*'
          PERCENT AT ABOUT 2.5 AIR STOICHiOMETRY  AND 5.2 EOUCTOR  NLE  °H   KNG  ?"u  OF ?HF hllNS
          MADE IN AUGUST WHEN THE  ROTARY DRUM FILTER WAS USED, THE FILTER CAKE SOLlis CONTFM
          AVERAGED 85 AND 86 PERCENT.                               riuitu LAKt SOLIDS CONTENT

          A TEN-DAY RUN WAS MADE  IN  SEPTEMBER ON  THE TCA SYSTEM WITH AUTOMATIC LIMESTONE FEFt) CON
          TROL BASED ON STOICHIOMETRY .   THE  LIMESTONE SLURRY FEED RATE WAS C                "

                                        " C°NCENTRAT ION«  THE «"«OL SYSTEM
OCT. 77   THE VENTURI/SPRAY  TOWER  SYSTEM CONTINUED TO OPERATED WITH TWO SCRUBBER STAGES  AND  FuRCED
NUV. 77   OXIDATION IN  THE VENTURI  HOLD  TANK.   IN OCTOBER, THE FOLLOWING IMPRUVtMENTS  WERE MADE WITH
          NO SIGNIFICANT DROP  IN OXIDATION EFFICIENCY AND WITH SATISFACTORY S02 REMOVAL  EFFICIENCY
             • THE SPRAY TOWER  GAS  VELOCITY WAS INCREASED FROM 6.7 TO 9.4 FT/SEC.        cr r int MI. T .
             •THE OXIDATION  TANK LEVEL  WAS DROPPED FRUM 18 FT TO la FT.
             *TME AIR SPARGER  RING,  CONTAINING no IM-INCH DIAMETER HOLES,  WAS REPLACED  WITH  A
              SINGLE 3-INCH  DIAMETER PIPE DISCHARGING DOWNWARD AT THE CENTER OF THE  OXIDATION  TANK
              3 INCHES  FROM  THE BOTTOM.
          WITH AIR DISCHARGED  FROM  AN OPEN-ENDED PIPE IT WAS APPARENT THAT  AIR DISPERSION IN  THE
          OXIDATION TANK WAS  ACCOMPLISHED MAINLY BY  THE TURBINE AGITATOR RATHER THAN THE SPARGER.
          IN NOVEMBER,  A ONE-MONTH  RELIABILITY TEST  WAS STARTED ON THE VENTUFU/SPRA Y TOWER SYSTEM
          USING FORCED  OXIDATION WITH TWO SCRUBBER STAGES AND LIMESTONE SLURRY WITH  HIGH FLY  ASH
          LOADING.  THE FLUE  GAS RATE TO THE SCRUBBER SYSTEM WAS VARIED ACCORDING TO THE bOILER LUAD
          WHICH RANGED  BETWEEN 100  AND  155 MW.  TEST CONDITIONS WERE SELECTED TO MEET  THE EPA  NEW
          SOURCE PERFORMANCE  STANDARDS  OF 1.2  LBS S02 AND 0.1 LB PAKTICULATE PER MILLION BTU.   THIS
          RUN WAS STILL IN PROGRESS AT  THE END OF NOVEMBER.  ON THE TCA SYSTEM, FORCED OXIDATION
          WITH A SINGLE SCRUBBER STAGE  USING AN AIR  EDUCTOR WAS DISCONTINUED IN EAhLV  OCTOBER  AFTtR
          A HOLE ERODED THROUGH THE EDUCTOR BODY.  FORCED OXIDATION TESTING WILL BE  RESUMED  IN  EARLY
          DECEMBER AFTER AN  AIR SPARGER  IS INSTALLED.
          IN OCTOBER-NOVEMBER,  A ONE-MONTH RELIABILITY TEST WITHOUT FORCED  OXIDATION WAS CONDUCTED
          ON THE TCA SYSTEM  WITH LIMESTONE SLURRY, FLUE GAS WITH HIGH FLY ASH LOADING, THREE  HOLD
          TANKS IN SERIES, AND 7.5  INCHES STATIC HEIGHT OF NITRILt FOAM SPHERES IN EACH  UF 3  BEOS IN
          THE TCA.  GAS RATE  TO THE SCRUBBER WAS VARIED WITH BOILER LOAD AND STOICHIOMETRIC  RATIU
          WAS CONTROLLED BY  AN AUTOMATIC LIMESTONE FEED SYSTEM.  CONDITIONS WERE SELECTED TO  MEET
          THE EPA NEW SOURCE  PERFORMANCE STANDARDS AT A LOW STOICHIOMETRIC  RATIO OF  1 .2  MOLES  CA/
          MOLE 302 ABSORBED.   THE  AVERAGE SU2  REMOVAL FOR THE ENTIRE RUN WAS 86 PERCENT  AT 2800 PPM
          WHICH WAS BETTER THAN THE 83  PERCENT REQUIRED TO MEET TEHE EMISSIONS STANDARD.  HOWEVER,
          THE STANDARD  WAS FREQUENTLY EXCEEDED FOR PERIODS GREATER IHAN THE 3 HOURS  ALLOWED  BY  THE
          EPA REGULATIONS.   AVERAGE OUTLET PARTICULATE MASS LOADING WAS 0.043 GRAIN/SCF  DRY  WHICH
          WAS BETTER THAN  THE 0.052 GRAIN/SCF  DRY CAT 30 PERCENT EXCESS AIR) REQUIRED  TO MEET  THE
          STANDARD.  THE RANGE OF  THE OUTLET MASS LOADING WAS 0.026 TO 0.069 GRAIN/SCF DRY.

 DEC.  77   A LIMESTONE RELIABILITY  TEST  ON THE  VENTURI/SPRAY TOWER SYSTEM WAS COMPLETED IN MID-
 JAN.  78   DECEMBER, 1977 AFTER 965 OPERATING HOURS.   THE TEST WAS CONDUCTED WITH TWO SCRUBBER
          LOOPS WITH FORCED  OXIDATION IN THE FIRST (VENTURIS LOOP.  THE FLUE GAS FLOW  RATE WAS
          VARIED ACCORDING TO THE  BOILER LOAD  WHICH  RANGED BETWEEN 100 AND  155 MW.
          TEST CONDITIONS  WERE SELECTED  TO MEET THE  EPA NEW SOURCE PERFORMANCE STANDARDS OF
          1.2 LB S02 AND 0.1  LB PARUCULATE PER MILLION BTU.  THE OPERATING RELIABILITY  OF THE
          SYSTEM WAS DEMONSTRATED.   HOWEVER, DUE TO  WIDE VARIATION IN THE INLET 302  CONCENTRA-
          TION  C2500-3aOO  PPM) AND THE  SLOW SYSTEM RESPONSE TIME, THE 302 EMISSION STANDARD  WAS
          FREQUENTLY EXCEEDED FOR  PERIODS GREATER THAN THE THREE HOURS ALLOWED BY EPA  REGULA-
          TIONS.  AVERAGE  S02 REMOVAL FOR THE  ENTIRE RUN WAS 86 PERCENT AT  2950 PPM  AVERAGE
          INLET S02, WHICH WAS HIGHER THAN THE 8« PERCENT REQUIRED TO MEET  THE STANDARD  FOR
          2800 PPM INLET S02.   THE OUTLET PARTICULATE LOADING RANGED FROM 0.021 TO 0.063
          GRAIN/DRY SCF, WITH A RUN AVERAGE OF 0.042 GRAIN/DRY SCF.  THESE  VALUES COMPARE WITH
          A LOADING OF  0.052 GRAIN/DRY  SCF OR  LESS REQUIRED TO MEET THE EPA PARTICOLATE  STAN-
          DARD, ASSUMING 30  PERCENT TOTAL BOILER EXCESS AIR.

          ANOTHER RELIABILITY RUN  ON THE VENTURI/SPRAY TOWER SYSTEM WAS STARTED IN MID DECEMBER
          USING LIME SCRUBBING.   THE RUN WAS COMPLETED IN JANUARY 1978.  WITH THE EXCEPTION  OF
          HIGHER SPRAY  TOWER  INLET  PH AND HIGHER ALKALI UTILIZATION INHERENT WITH THE  LIME
          SYSTEM, THE OPERATING CONDITIONS AND THE TEST RESULTS WERE SIMILIAR TO THOSE UF  THE
          LIMESTONE RELIABILITY RUN.

          ON THE TCA SYSTEM,  TWO RUNS WERE MADE WITH THE NITRILE FOAM SPHERES REPLACED BY  A  46
          INCH HEIGHTH  123 LAYERS)  OF CEILC01E PACKING SUPPORT PLATES.  AT  FULL GAS FLOW RATE
          OF 30,000 ACFM,  THE S02  REMOVAL FOR  THE CEILCOTt PLATES WAS SLIGHTLY LESS THAN THAT
          OF A 3-BED, 4-GRID TCA WITH FIVE INCHES OF STATIC SPHERE HEIGHT "H BED.  HO«£VER,
          AT 18,000 ACFM,  THE SU2  REMOVAL FOR  THE CEILCOTE PLATES WAS A FEW PERCENTAGE POINTS
          HIGHER THAN EXPERIENCED  WITH  THE TCA BEDS.
          FORCED  OXIDATION  TESTS WERE CONDUCTED ON THE TCA SYSTEM WITH AN *«
          LIMESTONE  SLURRY  WITH HIGH FLY ASH LOADING.  BOTH ONE-TANK CAIR SPARGING AND LIME-
                                                  139

-------
TENNESSEE VALLEY AUTHORITY                                       SHAWNEE UNIT NOS. 10A AND  1UB
          STONE ADDITION IN THE SAME TANK) AND TWO-TANK (AIR SPARGING IN THE F IRST !*£[* .
          LIMESTONE AUDITION IN THE SECOND) CONHGURAT IONS WERE USED.  NEAR COMPLfc ]*
          OXIDATION WAS ACHIEVED IN BOTH CONFIGURATION AT  AN AIH STUICHIOMETRT OF i.o
          OXYGEN/MOLE S02 ABSORBED AND OXIDATION TANK PH OF 5.1-5.7.  THE OXIDATION TANK LtVtL
          WAS 18 FT.
                                                  140

-------
                  TABLE 3
PERFORMANCE DESCRIPTION FOR OPERATIONAL  FGO  SYSTEMS THROUGH  01/78
 UTILITY NAME

 UNIT NAME

 UNIT LOCATION

 UNIT RATING

 FUEL CHARACTERISTICS

 FGD VENDOR

 PROCESS

 NEW OR RETROFIT

 START UP DATE

 FGD STATUS

 EFFICIENCY,
  PARTICULATES
 TENNESSEE VALLEY AUTHORITY

 WIDOWS CREEK NO. 6

 BRIDGEPORT ALABAMA

  550 MW

 COAL   3.7 PERCENT SULFUR

 TENNESSEE VALLEY AUTHORITY

 LIMESTONE SCRUBBING

 RETROFIT

  b/77

 OPERATIONAL


 99.5 PERCENT
   SOS
                        80  PERCENT
  MATER MAKE UP
  SLUDGE DISPOSAL
 100-ACRE DIKED POND
  UNIT COST
SEE APPENDIX A, FGD SYSTEM ECONOMICS
  OPERATIONAL
   EXPERIENCE
 REFER TO THE BACKGROUND INFORMATION SECTION IN TABLE 5 OF THIS REPORT.
 THE EMISSION CONTROL SYSTEM FOR THIS 550-MW COAL-FIRED POnER-GENERATING
 UNIT CONSISTS OF EXISTING ELECTROSTATIC PKECIPITATOKS FOLLOWED bY  FOUR
 PARALLEL SCRUBBING TRAINS, EACH CAPABLE OF HANDLING 25 PERCENT OF  THE
 BOILER FLUE GAS FROM UNIT NO. 6. EACH  TRAIN INCLUDES A RECTANGULAR-
 THROAT VENTURI SCRUBBER AND A GRID-TOWER ABSORBER SUPPLIED BY  POLYGON.
 THE GRID TOWER CAN BE CONVERTED TO A MOblLE-BED TOWER IF GREATER S0£ RE-
 MOVAL IS REQUIRED.
                                               141

-------
                                       BACKGROUND  INFORMATION
                                                 ON
                                         WIDOWS CKEEK NO. &

     IN MID-1970, TENNESSEE VALLEY AUTHORITY DECIDED TO  INSTALL  A FULL-SCALE  DEMONSTRATION LIMESTONE
SCRUBBING S02 REMOVAL SYSTEM ON GENERATING UNIT NO. 8 AT THE WIDOWS CHEEK  PLANT.   THE PRIMARY
OBJECTIVE WAS TO WORK OUT DESIGN AND OPERATING PROBLEMS  IN S02 REMOVAL OPERATIONS  AS  A PREPARATION
FOR THE POSSIBILITY OF FUTURE TVA F6D OPERATIONS.

     THE WIDOW CREEK POWER STATION IS LOCATED IN NORTHEAST ALABAMA, NEAR CHATTANOOGA,  TENNESSEE.
UNIT NO. 8 IS A COAL-FIRED BOILER WITH A MAXIMUM GENERATING CAPACITY OF 550 MW, AND A  MAXIMUM STACK
GAS RATE OF 1,600,000 CFM AT £80 DEGREES F.  THE BOILER  AND ESP  UNITS WERE COMMISSIONED BY TVA IN
1963.

     THE WET LIMESTONE FGD SYSTEM AT WIDOWS CREEK WAS PLACED IN  SERVICE ON MAY  16,  19/7.   THE SYSTEM
CONSISTS OF FOUR IDENTICAL SCRUBBING MODULES (IDENTIFIED AS A, B, C, AND D) EACH HANDLING  25 PERCENT
OF THE FLUE GAS FROM UNIT NO. 8.  LIMESTONE STORAGE AND  MILLING  FACILITIES AND  A SLUDGE DISPOSAL
POND ARE ALSO LOCATED ON SITE.

     FLUE GAS ENTERING THE SCRUBBING MODULE FROM THE EXISTING ELECTROSTATIC PRECIPITATORS  PASSES
THROUGH A «00,000 ACFM CAPACITY F.D. FAN AND INTO THE VENTURI.   THE VENTURI SCRUBBER  IS A  REC-
TANGULAR THROAT DESIGN USED TO SATURATE, AND REMOVE FLYASH FROM  THE GAS.   DUE  TO THE  INEFFICIENCY OF
THE OLD ESP UNITS, LARGE VENTURI SCRUBBERS WERE REQUIRED IN ALL  MODULES TO REMOVE  PARTICULATES.   302
REMOVAL EFFICIENCY IN THE VENTURI IS ABOUT 10 PERCENT.   THE ABSORBER IS A  GRID  TYPE ABSORPTION TOWEK
WHICH WAS SUPPLIED BY POLYGON.  THE GRID TOWER WILL BE USED INITIALLY AS A SPRAY TOWER  AND WILL
OPERATE AT A LIQUID-TO-GAS RATIO OF 50.  THE S02 REMOVAL EFFICIENCY FOR THE ABSORBER  IS ABOUT 70X,
GIVING A COMBINED SCRUBBER DESIGN EFFICIENCY OF ABOUT 80 PERCENT FOR THE ABSORBER  AND  VENTURI
TOGETHER.  THE ENTRAINMENT SEPARATOR IS A CHEVRON VANE TYPE U PASS) LOCATED  VERTICALLY IN A HORI-
ZONTAL SHELL.  THE REHEAT SYSTEM CONSISTS OF A STEAM/HOT AIR INJECTION SYSTEM RAISING  THE  FLUE GAS
TO AN OUTLET TEMPERATURE OF 175 F.

     LIMESTONE HANDLING AND MILLING EQUIPMENT INCLUDES A SHAKER  FOR TRUCK  AND RAIL UNLOADING,  A LIVE
STORAGE SILO, A WET BALL MILL, AND A CYCLONE CLASSIFIER.  THE GRINDING SYSTEM  IS DESIGNED  TO PRODUCE
A GROUND PARTICLE SIZE OF 90 PERCNET MINUS £00 MESH AT THE DESIGN RATE OF  50  TONS  PER  HOUR DRY
LIMESTONE.  THE UNLOADING AND STORAGE FACILITIES UP TO AND INCLUDING THE LIVE STORAGE  SILO ARE DE-
SIGNED TO ACCOMODATE A FUTURE LIMESTONE SCRUBBING FACILITY ON WIDOWS CREEK UNIT NO. 7.

     WASTE BY-PRODUCT SOLIDS FROM THE SCRUBBING FACILITY WILL BE DISPOSED  OF  IN A  DIKED POND 100
ACRES  IN AREA BY 30 FEET IN HEIGHT.  AN ADDITIONAL 10 FEET IN HEIGHT MAY BE ADDED  TO  YIELD A TOTAL
SLUDGE STORAGE CAPACITY OF 5.a MM. CUBIC YARDS, OR 10 YEARS OF SCRUBBER EFFLUENT STORAGE.   THE
SLUDGE, CONSISTING OF FLYASH, REACTION PRODUCTS (HYDRATES OF CALCIUM SULFITE  AND SULFATE)  AND UN-
REACTED LIMESTONE IS PUMPED TO THE POND AS A 15-16 PERCENT SOLIDS SOLUTION.

     THE WIDOWS CREEK NO. 8 SCRUBBING UNIT IS DESIGNED TO BE AS  FLEXIBLE AS POSSIBLE.   A LARGE
RESERVOIR OF QUENCH WATER IS LOCATED ABOVE THE ABSORBER  TO GRAVITY FEED WATER TO THE  TOWER  IN CASE
OF POWER FAILURE, THEREBY SAVING THE ABSORBER AND RUBBER LINING.  THE ABSORBER  CAN BE  OPERATED AS A
MULTI-GRID, TURBULENT CONTACT, OR SPRAY TOWER ABSORBER.  PROVISIONS HAVE BEEN MADE IN  THE  ABSORBER
DESIGN SO THAT IT CAN READILY BE CONVERTED TO A MOBILE BED TYPE  ABSORBER SHOULD IT PROVE DESIRABLE
IN THE FUTURE TO OBTAIN IMPROVED S02 REMOVAL.

     ADDITIONAL INFORMATION AND DATA ARE PROVIDED IN THE PERFORMANCE HISTORY  TABLE THAT FOLLOWS.
A SCHEMATIC DIAGRAM OF THE WIDOWS CREEK SCRUBBER PLANT IS PROVIDED IN APPENDIX  B OF THIS REPORT.

•INITIAL OPERATING EXPERIENCE*

VIRTUALLY ALL MAJOR CONSTRUCTION ON THE SCRUBBER PLANT WAS COMPLETED DURING THE FIRST  QUARTER OF
1977.  STARTUP AND SHAKEDOWN PROCEDURES COMMENCED OFFICIALLY ON  APRIL 30,  1977.  OPERATIONS  DURING
THIS INITIAL MECHANICAL SHAKEDOWN AND DEBUGGING PHASE OF OPERATIONS FOR THIS  FOUR  TRAIN WET  LIME-
STONE  SCRUBBING SYSTEM CONTINUED THROUGHOUT THE SUMMER.  COMMERCIAL SCRUBBER  PLANT OPERATION COM-
MENCED SOMETIME IN LATE SEPTEMBER.  THE UTILITY REPORTED A NUMBER OF PROBLEMS WITH BOTH THE  BOILER
SIDE AND THE SCRUBBER SIDE.  ALL FOUR SCRUBBER MODULES HAD NOT BEEN IN SERVICE  SIMULTANEOUSLY.
                                                 142

-------
TENNESSEE VALLEY  AUTHORITY


 
-------
                  TABLE 3
PERFORMANCE DESCRIPTION FOk OPERATIONAL  FGD  SYSTEMS  THROUGH   01/78
 UTILITY NAME

 UNIT NAME

 UNIT LOCATION

 UNIT RATING

 FUEL CHARACTERISTICS

 FGO VENDOR

 PROCESS

 NEW OR RETROFIT

 START UP DATE

 FGD STATUS

 EFFICIENCYr
   PARTICULATES
 TEXAS  UTILITIES CO.

 MARTIN LAKE  NU. 1

 TATUM  TEXAS

  793 MW

 COAL    1.0 PERCENT  SULFUR

 RESEARCH COTTRELL

 LIMESTONE SCRUBBING

 NEW

  6/77

 OPERATIONAL


 99.
-------
                                       BACKGROUND  INFORMATION
                                                 ON
                                        MARTIN  LAKE  NO,  1
INITIAL  OPERATING EXPERIENCE
THE  INSTALLATION OF THE LIMESTONE SCRUBBING  SYSTEM  AND  THE  ESP  HAS  OVER  IN  OCTDBFR  77 4s srncnm Pn
THE  UTILITY  HAS EXPERIENCED SOME DIFFICULTIES  !N  THt  SLUHHY  HANDLING  SYSTEM?   ?HE  IN TUL OPIATING
PHASE  IS  EXPECTED TO CONTINUE THROUGH FIRST  UUANTER OF  77.   COMPLIANCE  TEST NG  WAS  CONDUCTED IN
LATE 77,  AND CERTIFICATION OF COMMERCIAL  AVAILABILITY  IS  AWAITED        '"'^6  rtAS  CONDUCTED IN
                                                 145

-------
                                         TABLE  «
                                SUMMARY OF FGO  SYSTEMS BY  COMPANY
                                                                  •STATUS-
         UTILITY
ALABAMA ELECTRIC COOP
ALLEGHENY POWER SYSTEM
ARIZONA ELECTRIC POWER COOP
ARIZONA PUBLIC SERVICE
BASIN ELECTRIC POWER COOP
BIG RIVERS ELECTRIC COOP CORP.
BOARD OF MUNICIPAL UTILITIES
BRAZOS ELECTRIC POWER COOP
CENTRAL ILLINOIS LIGHT CO.
CENTRAL ILLINOIS PUBLIC SERV
CENTRAL MAINE POWER CO.
CINCINNATI GAS & ELECTRIC CO.
COLORADO UTE ELECTRIC ASSN.
COLUMBUS & SOUTHERN OHIO ELEC.
COMMONWEALTH EDISON
DELMARVA POWER CO.
DUQUESNE LIGHT
EASTERN KENTUCKY POWER COOP
HOOSIER COOPERATIVE
INDIANAPOLIS POWER & LIGHT CO.
KANSAS CITY POWER & LIGHT
KANSAS POWER & LIGHT
KENTUCKY UTILITIES
LAKELAND UTILITIES
LOUISVILLE GAS & ELECTRIC
MINNESOTA POWER AND LIGHT CO.
MINNKOTA POWER COOPERATIVE
MONTANA POWER CO.
NEVADA POWER
NEW ENGLAND ELEC SYSTEM
NIAGARA MOHAWK POWER COOP.
NORTHERN INDIANA PUB SERVICE
NORTHERN STATES POWER CO.
OTTER  TAIL POWER COMPANY
PACIFIC GAS AND ELECTRIC
PACIFIC POWER AND LIGHT CO.
PENNSYLVANIA POWER CO.
PHILADELPHIA ELECTRIC CO.
PUBLIC SERVICE CO OF NEW MEX.
PUBLIC SERVICE OF INDIANA
SALT RIVER PROJECT
SOUTH  CAROLINA PUBLIC SERVICE
SOUTHERN ILLINOIS POWER COOP
SOUTHERN INDIANA GAS&ELECTRIC
SOUTHERN MISSISSIPPI ELECTRIC
SPRINGFIELD CITY UTILITIES
SPRINGFIELD WATER  LIGHTSPOWER
TENNESSEE VALLEY AUTHORITY
TEXAS  MUNICIPAL POWER AGENCY
TEXAS  POftEK AND LIGHT CO.
TEXAS  UTILITIES CO.
UNITED POWER ASSOCIATION
UTAH POWER & LIGHT CO.
WISCONSIN POWER & LIGHT CO.
TOTAL
OPERATIONAL CONSTRUCTION
CONTRACT PLANNE
AWARDED
NO
2
2
2
8
5
2
1
1
2
1
I
1
2
4
1
1
2
1
2
2
3
4
1
1
6
1
1
4
10
1
1
3
4
1
2
1
3
4
It
1
3
2
1
1
2
1
1
4
1
3
b
2
2
1
MW
450.
1250.
400.
2804.
2550.
490.
235.
400.
800.
575.
600,
600.
900.
1550.
425.
180.
920.
500.
980.
1060.
1060.
1885.
64.
350.
2283.
500.
450.
2120.
3000.
650.
100.
705.
3140.
400.
1600.
509.
2475.
646.
1715.
650.
1050.
580.
184.
250.
360.
200.
190.
1115.
400.
2045.
4672.
1090.
815.
527.
NO
0
0
0
1
0
0
0
0
0
0
0
0
0
1
0
0
2
0
0
1
3
2
1
0
2
0
1
2
3
0
0
1
2
0
0
0
2
1
0
0
0
1
0
0
0
1
0
3
0
0
1
0
0
(1
MW
0.
0.
0.
115.
0.
0.
0.
0.
0.
0.
0.
0.
0.
400.
0.
0.
920.
0.
0.
530.
1060.
525.
64.
0.
243.
0.
450.
720.
375.
0.
0.
115.
1420.
0.
0.
0.
1650.
120.
0.
0.
0.
280.
0.
0.
0.
200.
0.
570.
0.
0.
793.
0.
0.
0.
NO
2
2
2
1
0
2
0
1
1
1
0
0
2
1
1
1
0
0
0
0
0
2
0
0
4
0
0
0
0
0
0
0
0
0
0
1
0
0
2
0
0
0
1
1
2
0
0
0
0
1
1
2
2
0
MW
450.
1250.
400.
250.
0.
490.
0.
400.
400.
575.
0.
0.
900.
400.
425.
180.
0.
0.
0.
0.
0.
1360.
0.
0.
1380.
0.
0.
0.
0.
0.
0.
0.
0.
0.
0.
509.
0.
0.
715.
0.
0.
0.
184.
250.
360.
0.
0.
0.
0.
545.
2336.
1090.
815.
0.
NO
0
0
0
1
2
0
1
0
0
0
0
1
0
0
0
0
0
0
0
0
0
0
0
0
0
1
0
2
0
0
1
0
2
1
0
0
1
0
0
0
2
0
0
0
0
0
1
1
1
0
1
0
0
1
MW
0.
0.
0.
350.
1100.
0.
235.
0.
0.
0.
0.
600.
0.
0.
0.
0.
0.
0.
u.
0.
0.
0.
0.
0.
0.
500.
0.
1400.
0.
0.
100.
0.
1720.
400.
0.
0.
825.
0.
0.
0.
700.
0.
0.
0.
0.
0.
190.
575.
400.
0.
793.
0.
0.
527.
NO
0
0
0
5
3
0
0
0
1
0
1
0
0
2
0
0
0
1
2
1
0
0
0
1
2
0
0
0
7
1
0
2
0
0
2
0
0
3
2
1
1
1
0
0
0
0
0
0
0
2
1
0
0
0
MW
0.
0.
0.
2089.
1450.
0.
0.
0.
40U.
0.
600.
0.
0.
750.
0.
0.
0.
500.
960.
530.
0.
0.
0.
350.
660.
0.
0.
0.
2625.
6bO.
0.
590.
0.
0.
1600.
0.
0.
726.
1000.
650.
350.
300.
0.
0.
0.
0.
0.
0.
0.
1500.
750.
0.
0.
0.
   TOTALS
                                131  55679.  31  10550.  38   15661.  20   10115.   42   19050.
    NOTE - PLANNED STATUS INCLUDES LETTER OF IlMTENT SIGNED, REQUESTING/EVALUTING  BIDS,
           AND CONSIDERING ONLY FGU SYSTEMS
                                                 146

-------
                                    TABLE 5
                        SUMMARY OF FGO SYSTEMS  BY  VENOUR

TOTAL
MANUFACTURER/PROCESS
AOL/COMBUSTION EQUIP ASSOCIATE
DOUBLE ALKALI SCRUBBING
LIME/ALKALINE FLYASH SCRUBBING
SODIUM CARBONATE SCRUBBING
TOTAL -
AMERICAN AIR FILTER
LIME SCRUBBING
TOTAL -
ATOMICS INTERNATIONAL
AQUEOUS CARBONATE SCRUBBING
TUTAL -
BA6COCK & WILCOX
LIME SCRUBBING
LIMESTONE SCRUBBING
TOTAL -
BUELL/ENVIROTECH
DOUBLE ALKALI SCRUBBING
TOTAL -
CHEMICO
LIME SCRUBBING
LIME/ALKALINE FLYASH SCRUBBING
LIME/LIMESTONE SCRUBBING
LIMESTONE SCRUBBING
TOTAL -
COMBUSTION ENGINEERING
LIME SCRUBBING
LIMESTONE SCRUBBING
TOTAL -
DAVY POWERGAS
WELLMAN LORD
TOTAL -
DAVY POWERGAS/ALLIED CHEMICAL
WELLMAN LORD/ALLIED CHEMICAL
TOTAL -
FMC CORPORATION
DOUBLE ALKALI SCRUBBING
TOTAL -
PEABOOY ENGINEERING
LIME/ALKALINE FLYASH SCRUBBING
LIMESTONE SCRUBBING
TOTAL -
PULLMAN KELLOGG
LIME SCRUBBING
LIMESTONE SCRUBBING
TOTAL -
RESEARCH COTTRELL
LIMESTONE SCRUBBING
TOTAL -
"ILEY STOKER / ENVIRONEERING
LIMESTONE SCRUBBING
TOTAL -
NO.

1
5
3
9

b
6

1
1

3
5
8

1
1

b
1
1
1
9

b
11
17

1
1

3
3

1
1

1
4
5
1
2
3
12
12
3
3
M\N

£77.
2570.
375.
3222.

1652.
1652.

100.
100.

1B50.
1919.
37b9.

575.
575.

3385.
527.
10.
750.
1672.

1570.
6545.
8123.

180.
180.

830.
830.

250.
250.

500.
1350.
1850.
825.
700.
1525.
5577.
5577.
760.
760.
OPERATIONAL
NO.

0
3
3
6

2
2

0
0

0
2
2

0
0

4
0
1
0
5

3
4
7

0
0

1
1

0
0

0
0
0
0
0
0
2
2
0
0
MW

0.
1170.
375.
1515.

242.
242.

0.
0.

0.
1100.
1100.

0.
0.

2570.
0.
10.
0.
2580.

305.
1945.
2250.

0.
0.

115.
115.

0.
0.

0.
0.
0.
0.
0.
0.
908.
908.
0.
0.
CufxSTkUCTIUN
WO.

1
0
0
1

4
4

0
0

2
2
4

1
1

2
U
u
1
3

3
3
b

1
1

2
2

1
1

0
4
4
0
0
0
5
5
3
3
MA

277.
0.
0.
277 .

1410.
1410.

0.
0.

1250.
584.
1834.

575.
575.

815.
0.
0.
750.
1565.

1273.
1905.
3178.

180.
180.

715.
715.

250.
250.

0.
1350.
1350.
0.
0.
0.
2236.
2236.
760.
760.
CONTKACf
AhA&DED
NO.

0
2
0
2

0
0

1
1

1
1
2

0
0

0
1
0
0
1

0
4
4

0
0

0
0

0
0

1
0
1
1
2
3
5
5
0
0
Mn

0.
1400.
0.
1400.

0.
0.

100.
100.

600.
235.
835.

0.
0.

0.
527.
0.
0.
527.

0.
2695.
2t>95.

0.
0.

0.
0.

0.
0.

500.
0 .
500.
825.
700.
1525.
2433.
2433.
0.
0.
TENNESSEE VALLEY  AUTHORITY
 LIMESTONE SCRUBBING
550.
         1    550.
                            0.
                                                  147

-------
                                     TABLE 5
                         SUMMARY OF FGD SYSTEMS BY VENDOR
                                             .	STATUS---	 —
                                    TOTAL    OPERATIONAL  CONSTRUCTION   CONTRACT
                                                                        AWARDED
     MANUFACTURER/PROCESS
                                 NO.
                                              NO.
                                                     MW
                                                           NO.
                                                                        MO.
TOTAL -                            1   550.     1   550.     0     0.     0      0.

UNITED ENGINEERS / PECO
 MAGNESIUM OXIDE SCRUBBING         1   120.     1   120.     0     0.     0      0.
TOTAL -                            i   120.     i   I2u.     o     o.     o      u.

UNIVERSAL OIL PRODUCTS
 LIME SCRUBBING                    2   800.     1   400.     1   400.     0      0.
 LIME/LIMtSlONE SCRUBBING          I    10.     1    10.     0     0.     0      0.
 LIMESTONE SCRUBBING               3  1155.     2   730.     1   425.     0      0.
 SODIUM CARBONATE SCRUBBING        i   bos.     o     o.     i   509.     o      o.
TOTAL -                            /  2474.     «  1140.     3  1331.     0      0.

WHEELABRATOR-FRYE/A.I.
 AQUEOUS CARBONATE/FAB. FILTER     1   400.     0     0.     0     0.     1   400.
TOTAL -                            1   400.     0     0.     0     0.     I   400.
                                  89 36629.
                                               31 10550.
                                                            3S 15664.
                                                                         £0 10415.
                                                  148

-------
 TABLE  fa
SUMMARY OF NEW AND RETROFIT FGO SYSTEMS bY
NEW OR OPERATIONAL CONSTRUCTION CONTRACT
PROCESS RETROFIT AWARDED

LIME SCRUBBING

LIME/ALKALINE FLYASH SCRUBBING

LIME/LIMESTONE SCRUBBING

LIMESTONE SCRUBBING

SUBTOTAL - LIME/LIMESTONE

AQUEOUS CARBONATE SCRUBBING

AQUEOUS CARBONATE/FAB. FILTER

DOUBLE ALKALI SCRUBBING

MAGNESIUM OXIDE SCRUBBING

NOT SELECTED

REGENERABLE NOT SELECTED

SODIUM CARBONATE SCRUBBING

WELLMAN LORD

WELLMAN LORD/ALLIED CHEMICAL

TOTALS
LIME/LIMESTONE % Of TOTAL MW

N
R
N
R
N
R
N
R
N
R
N
R
N
R
N
R
N
R
N
R
N
R
N
R
N
R
N
R
N
R
N
R
NU,
3
7
3
0
0
£
e
3
14.
12.
0
0
0
0
o
0
0
1
0
0
0
0
1
2
U
0
0
1
15.
16.

, MW
£050
1467
1170
0
0
20
14<43
790
7663.
2277.
0
0
0
0
0
0
0
120
0
0
0
0
125
250
0
0
0
115
77B8.
2762.
98
82
NU
11
1
0
0
0
0
18
1
29.
2.
0
0
0
0
2
1
0
0
0
0
0
0
I
0
0
1
1
1
33.
5.

. MM
4965
183
0
U
0
0
7585
425
12550.
boa.
0
0
0
0
825
277
0
0
0
0
0
0
509
0
0
160
375
340
14259.
1405.
86
43
NO
2
0
4
0
0
0
11
1
17.
1.
0
1
1
0
0
U
U
0
0
0
0
0
0
0
0
0
0
0
18.
2.

. MA
1425
U
2427
0
0
0
5488
575
9340.
575.
0
100
400
0
0
0
0
0
0
0
0
0
0
0
U
0
0
0
9740.
675.
96
85
PROCESS
PLANNED
NO
0
2
0
3
0
0
8
0
8.
5.
0
0
0
0
0
0
0
3
18
4
0
1
1
0
2
0
0
0
29.
13.

MM
0
fabu
U
579
0
0
4210
0
4210.
1239.
U
0
0
U
U
0
0
726
9000
2100
U
650
125
0
1000
0
a
0
14335.
4715.
29
26
TOTAL NO.
OF PLANTS
NO
16
10
7
3
0
2
45
5
66.
20.
0
1
1
U
2
1
0
U
IB
4
0
1
3
2
2
1
1
2
95.
36.

. Mrt
8440
2310
3597
579
0
2U
21726
1740
337b3.
4699.
U
100
4UO
0
825
2/7
U
8<46
9000
2100
0
650
759
250
1000
180
3/5
455
46122.
9557.
73
49
149

-------
                      TABLE  7
          SUMMARY OF  OPERATING  FGD  SYSTEMS  BY
          PROCESS AND  GENERATING  UNITS  AS OF  01/78
 PROCESS/GENERATING  UNITS
FGD/MW  STARTUP  EXPERIENCE(MO.)
LIME SCRUBBING
BRUCE MANSFIELD NO. 1
BRUCE MANSFIELD NO. 2
CANE RUN NO 4
CONESVILLE NO 5
ELRAMA POWER STATION
GREEN RIVER NOS. 1 2 AND 3
HAWTHORN NO. 3
HAWTHORN NO. 
-------
                             TABLE  8
        SUMMARY OF SLUDGt  DISPOSAL PRACTICES FOR OPERATIONAL FGD SYSTEMS  AS  OF   Ol/7a



PROCESS/GENERATING UNIT              "SLUDGE-      "SLUDGE	PQNQ	PuNO —
                                     STABILIZED    UNSTA61LIZEO        LINED          U^LIHtD


      LIME SCRUBBING

BRUCE MANSFIELD NO.  1                       825
BRUCE MANSFIELD NO.  2                       8£5
CANE RUN NO  4                               178                                            1?6
CONESV1LLE NO  5                             400                                            uun
ELRAMA POWER STATION                        510                                            5Ul
GREEN RIVER  NOS.  1   2   AND 3                                64                             b4
HAWTHORN NO. 3                                             iao                            lafl
HAWTHORN NO. 4                                             100                            luU
PADDYS RUN NO  6                              65                                             b5
PHILLIPS POWER STATION                     410                                            410

      TOTAL                                3213.            304.               0.           1867.

      LIME/ALKALINE  FLYASH SCRUBBING

COLSTRIP NO  1                                               360             360
.COLSTRIP NO  2                                               360                            360
MILTON R.  YOUNG  NO.  2                                       450

      TOTAL                                   0.           1170.             360.            360.

      LIMESTONE  SCRUBBING

CHOLLA NO  1                                                 115                            115
LA  CYGNE NO  i                                               820                            »20
LAWRENCE NO  4                                               125                            125
LAWRENCE NO  5                                               400                            400
MARTIN LAKE  NO.  1                          793                             793
PETERSBURG NO  3                             530                                            530
SHERBURNE  COUNTY  STATION NO.l                              710             710
SHERBURNE  COUNTY  STATION NO.2                              7io             7io
WIDOWS CREEK NO.  8                                         550                            550
WINYAH NO.  2                                               280                            280

      TOTAL                                1323.           3710.            2213.           262U,

      SODIUM CARBONATE SCRUBBING

REID GARDNER NO  1                                          l25
REID GARDNER NO  ^                                          1£5
REID GARDNER NO  3                                          125

      TOTAL                                   0-            375«               °'               °'
                                              151

-------
                                                 fABLt S
                               SUMMARY OF FGD SYSTEMS til PROCESS ANU REGULATORY  CLASS
REGULATORY OPERATIONAL
PROCESS CLA5S

LIME SCRUBBING




LIME/ALKALINE FLYASH SCRUBBING




LIME/LIMESTONE SCRUBBING




LIMESTONE SCRUBBING




SUBTOTAL - LIME/LIMESTONE




AQUEOUS CARBONATE SCRUBBING




AQUEOUS CARBONATE/FAB. FILTER




DOUBLE ALKALI SCRUBBING




MAGNESIUM OXIDE SCRUBBING





A
B
C
0
6
A
B
C
D
£
A
ti
C
D
E
A
B
C
0
E
A
B
C
U
E
A
B
C
0
E
A
B
C
0
E
A
B
C
D
E
A
B
C
U
E
NO.
0
8
2
0
0
0
3
0
0
0
0
0
2
0
0
4
5
2
0
0
4.
16.
6.
0.
0.
0
0
0
0
C
0
0
0
0
0
0
0
0
0
0
0
1
0
0
0
hrt
0
338b
129
0
o
(i
1170
0
0
0
0
0
20
0
0
iBOi
2060
1470
0
0
1603.
6618.
1519.
0.
0.
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
120
0
0
0
CONSTRUCTION
NU.
9
3
0
0
0
0
0
0
0
U
U
U
0
0
0
11
7
1
U
U
20.
10.
1.
0.
0.
0
0
0
0
0
0
0
0
0
0
2
1
0
0
0
0
0
0
0
0
MW
4140
100H
0
0
0
0
0
0
0
0
0
0
0
0
0
4675
2910
425
0
0
8815.
391B.
425.
0.
0.
0
0
0
0
0
0
0
0
0
0
825
277
0
0
0
0
0
0
U
0
CUNTKACT
AwAROtO
NO.
1
1
0
0
0
2
2
0
0
0
0
0
0
0
0
4
6
1
0
1
7.
9.
1.
0.
1.
0
0
1
0
0
0
1
0
0
0
0
0
0
0
0
0
0
0
0
0
M«v
600
825
0
0
0
1027
1400
0
0
0
0
0
0
0
0
1618
3520
575
0
350
3245.
5745.
575.
0.
350.
0
0
100
0
0
0
400
0
0
0
0
0
0
0
0
0
0
0
0
0
PLANNED
140.
0
2
0
0
0
0
3
0
0
0
0
0
0
0
0
5
3
0
(I
0
5.
8.
U.
0.
0.
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
3
0
0
0
My.
0
660
0
0
0
0
57S
0
0
0
0
0
0
0
0
2260
1950
0
0
0
2260.
3189.
u .
0.
U.
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
726
0
0
0
TOTAL NO.
PLAIMIS
NO
10
14
2
0
0
2
8
0
0
0
0
0
2
0
0
24
21
4
0
1
36.
43.
8.
0.
1.
0
0
1
0
0
a
i
0
0
0
i.
\
0
0
0
0
4
0
0
0
MW
4740
5881
129
0
0
1027
3149
0
0
u
u
0
2u
0
0
10356
10440
237U
0
350
16123.
19470.
2519.
0.
350.
0
0
100
0
0
0
400
0
0
0
B25
277
0
0
0
0
846
0
0
0
A.  BOILER CONSTRUCTED SUBJECT TO FEDERAL NSPS
B.  BOILER SUBJECT TO STATE STANDARD THAT IS MORE STRINGENT THAN THE FEDERAL NSPS
C.  BOILER SUBJECT TO STATE STANDARD THAT IS EQUAL TO OK LESS STRINGENT THAN NSHS
D.  OTHER
E.  REGULATORY CLASS UNKNUWN
                                               152

-------
                                             TABLE 9
                           SUMMARY OF FGO SYSTEMS BY PROCESS AND REGULATORY CLASS
REGULATOR
PROCESS CLASS

NOT SELECTED




RE6ENERABLE NOT SELECTED




SODIUM CARBONATE SCRUBBING




WELLMAN LORD




WELLMAN LORD/ALLIED CHEMICAL




TOTALS




LIME/STONE X OF TOTAL MW





A
b
c
0
E.
A
B
C
0
E
A
B
C
0
E
A
B
C
0
E
A
B
C
0
£
A
B
C
0
E
A
b
c
0
E
Y OPERA'
NO.
0
0
0
0
0
0
0
0
0
0
0
3
0
0
0
0
0
0
0
0
0
0
1
0
0
a.
20.
7.
0.
0.
100
93
93
0
0
TIONAL
MW
0
0
0
0
0
0
0
0
0
0
(J
375
U
0
0
0
0
U
b
0
0
0
115
0
U
1803.
7113.
1634.
0.
0.





CONSTRUCTION
NO.
0
0
0
0
0
0
0
0
0
0
0
1
0
0
0
0
0
1
0
0
0
2
0
0
0
22.
14.
2.
0.
0.





MW
0
0
0
0
0
0
0
0
0
0
U
509
0
0
0
0
0
160
0
0
0
71b
0
0
0
9640.
5419.
605.
0.
u .
91
72
70
0
0
CONTRACT
AWARDED
NO.
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
7.
10.
2.
0.
1.





MW
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
3245.
6145.
675.
0.
350.
100
93
85
0
100
PLANNED
NO.
7
13
2
0
0
0
0
1
0
0
U
1
0
0
0
0
2
0
0
0
0
0
0
0
0
12.
27.
3.
U.
0.





MW
4300
6210
59U
0
0
0
V
650
U
0
U
125
0
0
0
0
1000
U
U
0
0
0
0
0
U
6560.
1125U.
1240.
0.
0.
34
28
0
0
0
TOTAL NO.
PLANTS
NO
7
13
2
0
0
0
U
1
0
0
0
5
0
0
0
0
2
1
0
0
0
2
1
0
U
45.
71.
14
0
1





. MM
4300
621U
590
0
0
U
u
650
0
(1
(j
1009
0
0
U
0
1000
l«u
0
0
U
715
115
0
U
21248,
29927.
. 4154
0
350
76
65
61
0
100
A.

El
D.
E.
BOILER CONSTRUCTED SUBJEC1TO  FEDERAL  NSPS
BOILER SU^ECT IS BUTE SIS
OTHER
REGULATORY CLASS UNKNOWN
                                               smNGENT  THAN  THE  FEDERAL  NSPS
                                          "UAL  TO  OR  LESS  STRINGENT  THAN  NSPS
                                           153

-------
                      TABLE 10
            SUMMARY OF FGD SYSTEMS UNDER
CONSTRUCTION AS OF 01/78
       UTILITY COMPANY
        POWER STATION

ALABAMA ELECTRIC COOP
TOM8I6BEE NO. 2

ALABAMA ELECTRIC COOP
TOM8IGBEE NO. 3

ALLEGHENY POWER SYSTEM
PLEASANTS NO. 1

ALLEGHENY POWER SYSTEM
PLEASANTS NO. 2

ARIZONA ELECTRIC POWER COOP
APACHE NO i.

ARIZONA ELECTRIC POWER COOP
APACHE NO 3

ARIZONA PUBLIC SERVICE
CHOLLA NO 2

BIG RIVERS ELECTRIC COOP CORP.
REID NO. 2

BIG RIVERS ELECTRIC COOP CORP.
RE10 NO. 3

BRAZOS ELECTRIC POWER COOP
SAN MIGUEL NO. 1

CENTRAL ILLINOIS LIGHT CO.
UUCK CREEK NO. 1

CENTRAL ILLINOIS PUBLIC SERV
NEWTON NO.l

COLORADO UTE  ELECTRIC ASSN.
CRAIG NO. 1

COLORADO UTE  ELECTRIC ASSN.
CRAIG NO. 2

COLUMBUS & SOUTHERN OHIO ELEC.
CONESVILLE NO 6

COMMONWEALTH  EDISON
POWERTON NO.  51

DELMARVA PUWER CO.
DELAWARE CITY NOS. 1  2 & 3

KANSAS POWER  & LIGHT
JEFFERY NO.  1

KANSAS POWER  & LIGHT
JEFFERY NO.  2

LOUISVILLE GAS & ELECTRIC
CANE RUN NO  5

LOUISVILLE GAS & ELECTRIC
CANE RUN NO  6

LOUISVILLE GAS 8, ELECTRIC
MILL CREEK NU 3

LOUISVILLE GAS & ELECTRIC
MILL CREEK NO 4

PACIFIC POWER AND LIGHT CO.
JIM BRIOGER  NO. 4
NEW OR
RETROFIT
N
N
N
N
N
N
N
N
N
N
N
N
N
N
N
R
R
N
N
R
R
N
N
SIZE OF FGD
UNIT (MW)
225
225
625
625
200
200
250
250
240
400
400
575
450
150
100
125
180
680
680
183
277
125
495
PROCESS/VENDOR
PEABODY ENGINEERING
LIMESTONE SCRUBBING
PEABODY ENGINEERING
LIMESTONE SCRUBBING
BABCOCK & WILCOX
LIME SCRUBBING
BABCOCK 8, WILCOX
LIME SCRUBBING
RESEARCH COTTRELL
LIMESTONE SCRUBBING
RESEARCH COTTRELL
LIMESTONE SCRUBBING
RESEARCH COTTRELL
LIMESTONE SCRUBBING
AMERICAN AIR FILTER
LIME SCRUBBING
AMERICAN AIR FILTER
LIME SCRUBBING
BABCOCK & WILCOX
LIMESTONE SCRUBBING
RILEY STOKER / ENV IRONEER ING
LIMESTONt SCRUBBING
6UELL/ENVIROTECH
DOUBLE ALKALI SCRUBBING
PEABODY ENGINEERING
LIMESTONE SCRUBBING
PEABUDY tNGINtERING
LIMESTUNE SCRUBBING
UNIVERSAL OIL PRODUCTS
LIME SCRUBBING
UNIVERSAL OIL PRODUCTS
LIMESTONt SCRUBBING
DAVY PUWtRGAS
WELLMAN LORD
COMBUSTION ENGINEERING
LIMESTUNE SCRUBBING
COMBUST1UN ENGINEERING
LIMESTONE SCRUBBING
COMBUSTION ENGINEERING
LIME SCRUBBING
AOL/COMBUSTION EQUIP ASSUCIATE
DOUBLE ALKALI SCRUBBING
AMERICAN AIR FILTER
LIME SCRUBBING
AMERICAN AIR FILTER
START-UP
DATE
6/78
6/79
3/79
3/80
6/78
4/79
6/78
12/79
12/80
12/79
8/76
11/79
3/79
3/79
10/78
12/79
1/80
6/78
6/8U
4/78
11/79
1/78
b/80
             LIME SCRUBBING

    509      UNIVERSAL OIL PRODUCTS
             SODIUM CARBONATE SCRUBBING
9/79
                                                154

-------
                       TABLE  10
            SUMMARY  OF  FGO  SYSTEMS UNDER
       UTILITY COMPANY
        POWER STATION

PUBLIC SERVICE CD  UF NEW  MEX.
SAN JUAN NO.  1

PUBLIC SERVICE CO  OF NEW  MEX.
SAN JUAN NO.  i.

SOUTHERN ILLINOIS  POWER COUP
MARION NO.  4

SOUTHERN INDIANA  GAS&ELECTR1C
A.B. BROWN  NO.l

SOUTHERN MISSISSIPPI  ELECTRIC
R.D. MORROW NO.l

SOUTHERN MISSISSIPPI  ELECTRIC
R.D. MORROW NU.e

TEXAS  POWER AND  LIGHT  CO.
SANDOW  NO.4

TEXAS  UTILITIES  CO.
MARTIN  LAKE NO.  £

TEXAS  UTILITIES  CO.
MARTIN  LAKE NO.  5

TEXAS  UTILITIES  CO.
MONTICELLO NO.3

UNITED  POWtR ASSOCIATION
COAL  CREEK NO.  1

 UNITED  POWER ASSOCIATION
COAL  CREEK NO.  i.

 UTAH  POWER & LIGHT CO.
 EMERY  NO.l

 UTAH  POWER & LIGHT CO.
 HUNTINGTON NO.l
CONSTRUCTION AS OF 01/78

              PROCESS/VENDOR
NEW OK
RETROFIT
N
R
N
N
N
N
N
N
N
N
N
N
N
N
SIZE OF FGD
UNIT (Mrt)
375
340
184
2bO
160
180
545
7S3
793
' 750
545
545
400
415
DAVY POWERGAS/ALLIED CHEMICAL
WELLMAN LORD/ALLIED CHEMICAL

DAVY PUKtRbAS/ALLIED CHEMICAL
vJELLMAN LORD/ALLIED CHEMICAL

BABCOCK & WILCOX
LIMESTUNt SCKUdBING

FMC COHPURATION
DOUBLE ALKALI SCRUBBING

RILEY STOKER / ENV IRUNEEKING
LIMESTUNE SCRUBBING

WILEY STOKER / ENV I RONLtK ING
LIMESTUNt SCRUBBING

COMBUSTION ENGINEEKIiMG
LIMESTONc SCRUBBING

RESEARCH CUTTRELL
LIMESTONE SCRUBBING

RESEARCH CUTTHELL
LIMESTUNE SCRUBBING

CHEMICO
LIMESTONE SCRUBBING

COMBUSTION ENGINEERING
LIME SCRUBBING

COMBUSTION ENGINEERING
LIME SCRUBBING

CHEMICO
LIME SCRUBBING

CHEMICU
LIME SCRUBBING
                                            START-OP
                                               DATE

                                              -J/78


                                              7/78


                                              fa/78


                                              t/79


                                              5/7B


                                              8/78


                                              7/80
                                             12/78
                                             u/78


                                             11/79


                                             12/78


                                              "/78
                                                  155

-------
                   TABLE 11
            SUMMARY UK PLANNED FGD SYSTEMS AS UF 01/78
       UTILITY COMPANY
        POWER STATION
            CONTRACTS AWARDED

ARIZONA PUBLIC SERVICE
CHOLLA NO. 4

BASIN ELECTRIC POWER COOP
LARAMIE RIVER NO. 1

BASIN ELECTRIC POWER COOP
LARAMIE RIVER NO. 2

80ARO OF MUNICIPAL UTILITIES
SIKESTON POWER STATION

CINCINNATI GAS 5, ELECTRIC CO.
EAST BEND NO 2

MINNESOTA POWER AND LIGHT CO.
CLAY BOSWELL NO. 4

MONTANA POWER CO.
COLSTRIP NO. 3

MONTANA POWER CO.
COLSTRIP NO. 4

NIAGARA MOHAWK POWER COOP.
CHARLtS R. HUNTLEY NO.6

NORTHERN STATES POWER CO.
SHERBURNE COUNTY STATION NO.3

NORTHERN STATES POWER CO.
SHERBURNE COUNTY STATION NO.4

OTTER  TAIL POWER COMPANY
COYOTE NO. I

PENNSYLVANIA POWER CO.
BRUCE  MANSFIELD NO. 3

SALT RIVER PROJECT
CORONAUO NO.l

SALT RIVfcR PROJECT
CORONADO NO.2

SPRINGFIELD WATER  LIGHT&POWER
DALLMAN NO. 3

TENNESSEE VALLEY AUTHORITY
WIDOWS CREEK NO. 7

TEXAS  MUNICIPAL POWER AGENCY
GIBBUNS CREEK UNIT NO.  1

TEXAS  UTILITIES CO.
MARTIN LAKE NO. 4

WISCONSIN POWER & LIGHT CO.
COLUMBIA NO. 2
NEW OR
RETROFIT

N
N
N
N
N
N
N
H
N
N
N
N
N
N
N
R
N
N
N
SUE OF FGD
UNIT (MM)
350
550
550
235
600
500
700
700
100
860
860
400
825
350
350
190
575
400
793
527
          VENDOR/PROCESS                 START-UP
                                            UATE
         RESEARCH COTTRELL                6/80
         LIMESTONE SCRUBBING

         RESEARCH COTTRELL                1/80
         LIMESTONE SCRUBBING

         RESEARCH COTTRELL                10/80
         LIMESTONE SCRUBBING

         BA8COCK & WILCOX                 11/80
         LIMESTONE SCRUBBING

         BABCOCK & WILCOX                 1/81
         LIME SCRUBbING

         PEABODY ENGINEERING              0/80
         LIME/ALKALINE FLYASH SCRUBBING

         AOL/COMBUSTION EQUIP ASSOCIATE   7/80
         LIME/ALKALINE FLYASH SCRUBBING

         ADL/COMBUSTIUN EQUIP ASSOCIATE   7/dl
         LIME/ALKALINE FLYASH SCRUBBING

         ATOMICS INTERNATIONAL            0/80
         AQUEOUS CARBONATE SCRUBBING

         COMBUSTION ENGINEERING           5/81
         LIMESTONE SCRUBBING

         COMBUSTION ENGINEERING           5/83
         LIMESTONE SCRUBBING

         WHEELABRATOR-FRYE/A.I.           5/81
         AQUEOUS CARBONATE/FAB. FILTER

         PULLMAN KELLOGG                  4/80
         LIME SCRUBBING

         PULLMAN KELLOGG                  4/79
         LIMESTONE SCRUBBING

         PULLMAN KELLOGG                  4/80
         LIMESTONE SCRUBBING

         RESEARCH COTTRELL                7/80
         LIMESTONE SCRUBBING

         COMBUSTION ENGINEERING           O/ 0
         LIMESTONE SCRUBBING

         COMBUSTION ENGINEERING           1/82
         LIMESTONE SCRUBBING

         RESEARCH COTTRELL                11/82
         LIMESTONE SCRUBBING

         CHEMICO                          1/80
         LIME/ALKALINE FLYASH SCRUBBING
             LETTER  OF  INTENT SIGNED

 NEVADA  POWER
 RCIO  GARDNER  NO  4

 PHILADELPHIA  ELECTRIC  CO.
 EDDYSTONE  NO.  IB

 PUBLIC  SERVICE CO OF NEW MEX.
 SAN JUAN NO.  3
125      ADL/COMBUSTION EQUIP ASSOCIATE   O/ 0
         SODIUM CARBONATE SCRUBBING

240      UNITED ENGINEERS / PECO          6/80
         MAGNESIUM OXIDE SCRUBBING

500      DAVY POWERGAS                    1/79
         WELLMAN LORD
                                                156

-------
       TABLE 11
SUMMARY OF PLANNED FGD SYSTEMS AS UF 01/78
UTILITY COMPANY Nth OH
POWER STATION RETROFIT
REQUESTING/EVALUATING blOS
EASTERN KENTUCKY POWER COOP N
SPURLOCK GENERATING PLANT NO. 2
HOOSIER COOPERATIVE N
MEROM NO. 1
HOOSIER COOPERATIVE N
MEROM NO. 2
INDIANAPOLIS POWER & LIGHT CO. N
PETERSBURG NO 4
LAKELAND UTILITIES N
MCINTOSH POWER PLANT UNIT NO. 3
SOUTH CAROLINA PUBLIC SERVICE N
HINYAH NO. i
CONSIDERING FGD SYSTtM
ARIZONA PUBLIC SERVICE R
FOUR CORNERS NO. 1
ARIZONA PUBLIC SERVICE R
FOUR CORNERS NO. 2
ARIZONA PUBLIC SERVICE R
FOUR CORNERS NO. 3
ARIZONA PUBLIC SERVICE R
=OUR CORNERS NO. 4
ARIZONA PUBLIC SERVICE R
•OUR CORNERS NO. 5
JASIN ELECTRIC POWER COOP N
kNTELOPE VALLEY NO. 1
IASIN ELECTRIC POWER COOP N
INTELOPE VALLEY NO. 2
IASIN ELECTRIC POWER COOP N
.ARAMIE RIVER NO. 3
ENTHAL ILLINOIS LIGHT CO. N
UCK CREEK NO. 2
ENTRAL MAINE POWER CO. N
EARS ISLAND NO. 1
OLUMBUS & SOUTHERN OHIO ELEC. N
OSTON NO. 5
OLUMBUS & SOUTHERN OHIO ELEC. N
OSTON NO. 6
OUISV1LLE GAS & ELECTRIC R
ILL CREEK NO 1
3UISVILLE GAS & ELECTRIC H
ILL CREEK NO 2
•VAOA POWER N
»RRY ALLEN STATION NO. 1
:VAOA POWER N
>RRY ALLEN STATION NO. 2
VADA POWER N
SHE OF FGD
UNIT (MM)

500
490
490
530
350
300

175
175
229
755
755
150
450
550
100
600
375
375
330
330
500
500
500
VENDOK/PRUCESS

NOT SELECTED
NOT SELECTED
NOT SELECTED
LIMESTONE SCRUBBING
NOT SELECTED
LIMESTONE SCRUBBING
NOT SELECTED
LIMESTONE SCRUBBING
NOT SELECTED
LIMESTONE SCRUBBING
NOT SELECTED
NOT SELECTtD

CHEMICO/APS
LIME/ALKALINE FLYASH
CHEMICO/APS
LIME/ALKALINE FLYASH
CHEMICO/APS
LIME/ALKALINE FLYASH
NOT SELECTED
NOT SELECTED
NOT SELECTED
NOT SELECTED
NOT SELECTED
NOT SELECTED
NOT SELECTED
NOT SELECTED
NOT SELECTED
NOT SELECTED
NOT SELECTED
LIMESTONE SCRUBBING
NOT SELECTED
(MOT SELECTED
NOT SELECTED
NOT SELECTED
NOT SELECTED
NOT SELECTED
NOT SELECTED
LIME SCRUBBING
NOT SELECTED
LIME SCRUBBING
NOT SELECTED
NOT SELECTED
NOT SELECTED
NOT SELECTED
NOT SELECTED
NOT SELECTED
STAHT-UP
DATE

3/60
0/80
0/81
4/82
10/81
0/60

O/ 0
SCRUBBING
O/ 0
SCRUBBING
O/ 0
SCRUBBING
O/ 0
0/0
0/B1
0/83
6/8J
1/82
11/86
0/81
0/83
1/82
1/61
6/63
b/H4
6/85
                                    157

-------
                   TABLE 11
            SUMMARY OF PLANNED

       UTILITY COMPANY
        POWER STATION

NEVADA POWER
HARRY ALLEN STATION NO. 4

NEVADA POWER
WARNER VALLEY STATION NO. 1

NEVADA POWER
WARNER VALLEY STATION NO. 2

NEW ENGLAND ELEC SYSTEM
6RAYTON POINT NO.3

NORTHERN INDIANA PUB SERVICE
SAILLY NO. 7

NORTHERN INDIANA PUB SERVICE
BAILLY NO. 8

PACIFIC GAS AND ELECTRIC
FOSSIL NO. 1

PACIFIC GAS AND ELECTRIC
FOSSIL NO. 2

PHILADELPHIA ELECTRIC CO.
CROMBY

PHILADELPHIA ELECTRIC CO.
EOOYSTONE NO. 2

PUBLIC SERVICE CO OF NEW MEX.
SAN JUAN NO. «

PUBLIC SERVICE OF INDIANA
GIBSON 5

SALT RIVER PROJECT
CORONAUO NO.3

TEXAS POWER AND LIGHT CO.
TWIN OAKS NO. 1

TEXAS POWER AND LIGHT CO.
TWIN OAKS NO. 3

TEXAS UTILITIES CO.
FOREST GROVE NO. 1
FGD SYSTEMS AS OF 01/78
NEW OR
RETROFIT
N
N
N
R
R
H
N
N
R
R
N
N
N
N
N
N
SIZE OF FGD
UNIT (MW)
500
250
250
650
190
UOO
600
800
150
336
500
6bO
3SO
750
750
750
VENDOR/PROCESS
NOT SELECTED
NOT SELECTED
NOT SELECTED
NOT SELECTED
NOT SELECTED
NOT SELECTED
NOT SELECTED
REGENEkABLE NOT SELECTED
NOT SELECTED
NOT SELECTED
NOT SELECTED
NOT SELECTED
NOT SELECTED
LIMESTONE SCRUBBING
NOT SELECTED
LIMESTONE SCRUBBING
UNITED ENGINEERS / PECO
MAGNESIUM UXIDt SCRUBBING
UNITED ENGINEERS / PECO
MAGNESIUM OXIDE SCRUBBING
DAVY POWtRGAS
WELLMAN LORD
NOT SELECTED
NOT SELECTED
NOT SELECTED
LIMESTONE SCRUBBING
NOT SELECTED
NOT SELECTED
NOT SELECTED
NOT SELECTtD
NOT SELECTED
NOT SELECTED
                                                       3TART-UP
                                                          DATE

                                                         6/86
                                                         6/85


                                                         6/83


                                                         O/  0


                                                         O/  0


                                                         O/  0


                                                         0/8
-------
                      CONTENTS
                                  TABLE 12
       UTILITY COMPANY
        POWER STATION

ARIZONA PUBLIC SERVICE
FOUR CORNERS NO. 5A

BOSTON EDISON
MYSTIC NO 6

CENTRAL ILLINOIS LIGHT  CO.
DUCK CREEK NO. 1A

COMMONWEALTH EDISON
WILL COUNTY NO 1

OAIRYLANO POWER  COOP
ALMA STATION

DETROIT EDISON
ST. CLAIR NO 6

GULF POWER CO.
SCHOLZ NO. 1A

GULF POWER CO.
SCHOLZ NO. 3A

GULF POWER CO.
SCHOLZ NOS.  18 & 2B

ILLINOIS  POWER
WOOD RIVER NO  «

KEY WEST  UTILITY BOARD
STOCK  ISLAND  PLANT

POTOMAC ELECTRIC S POWER
OICKERSON NO.  3

PUBLIC SERVICE  CO OF COLORADO
VALMONT NO.  5

SOUTHERN  CALIFORNIA  tDISON
MOHAVE NO 1A

SOUTHERN  CALIFORNIA  EDISON
MOHAVE NO. 2A

TENNESSEE VALLEY AUTHORITY
SHAWNEE NO.   IOC

UNION  ELECTRIC  CO.
MEREMAC NO.  £
    SIZE OF FED  PROCESS/VENDOR
RETROFIT   UNIT  (MW)

     lb°      SO. CALIFORNIA EDISON
              LIME SCRUBBING

     ISO      CHEM1CO
              MAGNESIUM OXIDE SCRUBBING

     100      KILEY STOKER / ENV1RONEERING
              LIMESTONE SCRUBBING

     167      6ABCOCK & IVILCOX
              LIMESTONE SCRUBBING

      60      FOSTER WHEELER
              LIME INJECTION

     163      HEABODY ENGINEERING
              LIMESTONE SCRUBBING

      £0      ADL/COMBUSTION EUUIP ASSOCIATE
              DOUBLE ALKALI SCRUBBING

      20      FOSTER WHEELER
              ACTIVATED CAK80N

      23      CHIYODA INTERNATIONAL
              THOROUGHBRED 101

     110      MONSANTO ENVIRO CHEM SYSTEMS
              CATALYTIC OXIDATION

      37      ZURN AIR SYSTEMS
              LIMESTONE SCRUBBING

      95      CHEMICO
              MAGNESIUM OXIDE SCRUBBING

      50      UOP/PUB SERVICE OF COLORADO
              LIMESTUNE SCRUBBING

     170      UNIVERSAL OIL PRODUCTS
              LIMESTONE SCRUBBING

     160      SCE/STEAKNS ROGER
              LIME SCRUBBING

      10      TENNESSEE VALLEY AUTHORITY
              LIME/LIMESTONE SCRUBBING

     IHO      COMBUSTION ENGINEERING
              LIMESTONE INJECTION/WET SCRUB
PAGE  NO.


192


195


198


201


212


213


217


220


223


227


230


233


236


239


2*40


24«


246
                                                 159

-------
                 TABLE 12
DESCRIPTION OF TERMINATED FGU SYSTEMS  01/76
UTILITY NAME          ARIZONA PUBLIC SERVICE

UNIT NAME             FOUR CORNERS NO. 5A

UNIT LOCATION         FARMINGTON NEW MEXICO

UNIT RATING            160 MW

FUEL CHARACTERISTICS  CUAL  0.7 PERCENT SULFUR

FGO VENDOR            SO. CALIFORNIA EDISON

PROCESS               LIME SCRUBBING

NEW OR RETROFIT       RETROFIT

START  UP DATE          2/76

FGD STATUS            TERMINATED

EFFICIENCY,
 PART1CULATES


 soa


WATER  MAKE  UP


SLUDGE DISPOSAL


UNIT COST


OPERATIONAL           REFER TO  THE BACKGROUND  INFORMATION  SECTION  IN  TAbLE  12  OF  THE  REPORT.
 EXPERIENCE           THIS MOUULE WAS ORIGINALLY  INSTALLED  AT  THE  MQHAVE  GENERATING  STATION
                      AND OPERATED DURING THE  TEST MODULES  EVALUATION  PROGRAM.  THE  UNIT
                      WAS THEN  SHUTDOWN, MOVED FROM THE MOHAVE  TEST SITE,  AND  REASSEMBLED
                      AT  THE FOUR CORNERS STATION OF  APS.  THE  MODULE  WAS  IN  SERVICE  DURING
                      SEGMENTS  FROM FEB. 1976  TO  DEC. 6,  1976,  TREATING APPROXIMATELY  20  PER-
                      CENT OF THE FLUE GAS FLOW FROM  THE  75b-MW  RATEO  UNIT.  THE PROGRAM  HAS
                      BEEN TERMINATED AND THE  MODULE  DISASSEMBLED.
                                             160

-------
                                        BACKGROUND INFORMATION
                                                  ON
                       FOUR CORNERS  NO.  5*  - EXPERIMENTAL HORIZONTAL SCRUBBER

     THE  FOUR  CORNERS POWER STATION,  LOCATED NEAR FARMINGTON, NEW MEXICO, IS JOINTLY OWNED 8Y  THE
ARIZONA PUBLIC SERVICE COMPANY  AND  THE  SOUTHERN CALIFORNIA EDISON COMPANY.  THIS STATION CON A NS
FIVE  COAL-FIRED 801LEKS WITH  AN  EQUIVALENT  ELECTRIC POWER GENERATING CAPACITY OF 2233-M*.  ONLY UNIT
NO. 5 IS  RETROFITTED WITH AN  F60  SYSTEM.                                                   U L  U  *

     UNIT NO.  5 IS A COAL-FIRED  BOILER  CAPABLE OF GENERATING S,1<4,000 LBS. OF STEAM, WHICH IS  EQUI-
VALENT  TO 800-MW OF NET ELECTRICAL  POWER.  THIS UNIT WAS FIRST PLACED IN COMMERCIAL OPERAIION  JULY
1970.  APPROXIMATELY SO PERCENT  OF  THE  FLUE GAS GENERATED BY THIS BUILER IS BEING SCRUBBED INITIALLY
IN ORDER  TO ESTABLISH WHAT  SULFUR DIOXIDE AMD PARTICULATE REMOVAL EFFICIENCIES CAN BE ObTAIiMED.

     THE  FGO SYSTEM WHICH HAS BEEN  RETROFITTED ON UNIT NO. b IS THE WEIR HORIZONTAL CKOSSFLOW  SPRAY
SCRUBBER  WHICH WAS FORMERLY  INSTALLED AND OPERATED IN A TEST PROGRAM AT  THE MOHAVE GENERATING  STA-
TION  OF THE SOUTHERN CALIFORNIA  EDISON  COMPANY (SEE MOHAVE NO. 2A IN TABLE 16 OF THIS REPORT).

     DURING THE MOHAVE  TEST  PROGRAM THE HORIZONTAL MODULE WAS OPERATIONAL FROM NOVEMBER 1, 1973, TO
JANUARY 16,1974, FOR SHAKEDOWN PURPOSES.  OVER THE COURSE OF THE ACTUAL  TEST PROGRAM, WHICH EXTENDED
FROM JANUARY  16, 1974,  TO FEBRUARY  9, 1975, THE PROTOTYPE UNIT OPERATED  A TOTAL OF 5,927 HOURS IN
VARIOUS TEST  MODES.  FOLLOWING COMPLETION OF TESTS, THE MODULE WAS SHUT  DOWN, DISMANTLED, TRANSPORT-
ED,  AND REASSEMBLED  AT  THE  FOUR CURNERS GENERATING STATION OF ARIZONA PUBLIC SERVICE FOR FURTHER
TESTING.

     THE HORIZONTAL  MODULE  IS A FOUR-STAGE SCRUBBING CHAMBER WITH FOLLOWING DIMENSIONS!  LENGTH -  48
FEET, WIDTH •  28 FEET,  HEIGHT - Ib FEET.  THE MODULE ITSELF  IS A HOLLO*  CHAMBER CONSISTING OF  FOUR
STAGES OF  CROSSFLOW  SPRAY  NOZZLES.  EACH STAGE CONTAINS A ROW OF it> EXTERNALLY-MOUNTED NOZZLES.  THE
SLURRY IS  CYCLED  THROUGH  THE SCRUBBER IN A COUNTEKCURHENT MANNER AT A RATE OF 3b,000 GPM/STAGE,
FRESH LIME  SLURRY  IS  SPRAYED ACROSS THE FLUE GAS  AT THE FOURTH STAGE, WHICH IS  IHE DISCHARGE END OF
THE  SCRUBBING CHAMBER.   THE SCRUBBING SOLUTION IS THEN COLLECTED AND RECYCLED SUCCESSIVtLY TO  THE
THIRD, SECOND,  AND  FIRST  STAGES OF THE  SCRUBBING  MODULE.  THIS ALLOWS FOR COMPLETE DEPLETION OF ANY
EXCESS ALKALINITY  AND  INSURES THAT FRESH SLURRY  is CONTACTING GAS HAVING THE LOWEST SULFUR DIOXIDE
CONCENTRATION.   THE  LIQUID  RECIRCULAT ION RATE CAN BE ADJUSTED OVER A WIDE RANGE.  THE MODULE IS DE-
SIGNED TO  TREAT  A  MAXIMUM  FLUE GAS CAPACITY OF 450,000 SCFM.  THE DESIGN GAS VELOCITY THKOUfcH  THE
MODULE IS  21.6 FT/SEC.   THE CLEANED GASES THEN PASS THROUGH  A DEMISTER AND ARE REHEATED BEFORE BE-
 ING  DISCHARGED TO  THE  STACK.  THE SPENT SLURRY IS DISCHARGED FROM THE SCRUBBING SYSTEM TO A THICK-
ENER AND THE  UNDERFLOW  IS  PUMPED TO AN  ON-SITE SETTLING POND.  WATER IS  RETURNED TO THE PROCESS FOR
 FURTHER  USE.

      A CUTAWAY VIEW OF  THE  WEIR SCRUBBING CHAMBER  IS PRESENTED IN APPENDIX B.
                                                   161

-------
PERIOD

MONTH/YEAR
FEB. 76
MAR. 76
APR. 76
MAY  76
JUN. 76

JUU. 76
AUG. 76
SEP. 76

OCT. 76

NOV. 76
DEC. 76
       ARIZONA PUBLIC SERVICE
   OPERATING HOURS
BOILER     FGD SYSTEM
FOUH CORNERS UNIT NO. 5A


      COMMENTS
                          INSTALLATION OF THE MODULE AT THE FOUR CORNERS  GENERATING
                          STATION WAS COMPLETED AND THE MODULE hAS PLACED  IN-SERVICE
                          FEBRUARY 17, 1976, FOR INITIAL OPERATION.

                          THE SYSTEM WAS TAKEN DOWN IN MID-APRIL FOR A SCHEDULED  BOILER
                          OVERHAUL.

                          SYSTEM RESTART IS SCHEDULED FOR JULY 1976.
                          THE SYSTEM HAS REMAINED OUT OF SERVICE SINCE MID-APRIL  1976
                          BECAUSE OF AN EXTENSIVE OVERHAUL TO THE NO. 5 BOILER PLUS THE
                          DEVELOPMENT OF PROBLEMS WITH THE SCRUBBER MODULE'S REHEATER
                          UNIT.
                          THfc PROTOTYPE WAS IN SERVICE THROUGHOUT THE MONTH OF NOVEMBER.
                          ON DEC. fa THE TEST PROGRAM WAS CONCLUDED AND THE UNIT HAS
                          SINCE BEEN DISMANTLED.  APS IS NOrt IN THE PROCESS OF ANALYZING
                          THE OPERATING DATA ACCUMULATED DURING THE TEST PERIOD.  A RE-
                          PORT ADDRESSING THE RESULTS OF THE PROGRAM WILL BE PUBLISHED
                          IN FEBRUARY 1977.
                                                 162

-------
                 TABLE  12
DESCRIPTION OF TERMINATED  FGD SYSTEMS  01/78
UTILITY NAME

UNIT NAME

UNIT LOCATION

UNIT HATING

FUEL CHARACTERISTICS

FGD VENDOR

PROCESS

NEW OR RETROFIT

START  UP DATE

FGD STATUS

EFFICIENCY,
  PARTICULATES
BOSTON EDISUN

MYSTIC NO 6

EVERETT MASSACHUSETTS

 150 MH

OIL   2.5 PERCENT  SULFUR

CHEMICO

MAGNESIUM OXIDE  SCRUBbING

RETROFIT

 4/72

TERMINATED


50 PERCENT
  S02
                       90 PERCENT
 WATER  MAKE  UP
 SLUDGE  DISPOSAL
                       ACID PLANT REGENERATION
 UNIT  COST
                      SEE APPENDIX A, FGD SYSTEM ECONOMICS
 OPERATIONAL
  EXPERIENCE
REFER  TO  THE  BACKGROUND  INFORMATION  SECTION  IN  TABLE  12 OF  THIS REPORT.
THIS DEMONSTRATION  MAGNESIUM  OXIDE  SCRUBBER  PLANT  CONSISTED OF UNE SINGLE-
STAGE   VENTURI  MODULE  DESIGNED  BY CHEMICO.  THE  UNIT WAS ORIGINALLY PLACED
IN SERVICE  IN APRIL 1972.  TERMINATION  OF  THE DEMONSTRATION  PROGRAM OCCUR-
RED  IN  JUNE  1974.  FUNDING  FOR THE DEMONSTRATION PROGRAM WAS PROVIDED
PRIMARILY BY  THE  UTILITY  AND  EPA. THE  BOILER FIRED NO.6 HIGH  SULFUR RESID-
UAL  FUEL  OIL  DUK1NG THE  COURSE  OF THE  PROGRAM.  SYSTEM OPERA8ILITY  INDEX
VALUES  ARE  PROVIDED IN THE FOLLOWING TABLE
                                              163

-------
                                        BACKGROUND INFORMATION
                                                  ON
                               MYSTIC  NO.  b MAGNESIUM OXIDE SCRUBBER

     THE MAGNESIUM OXIDE-BASED  FGU  SYSTEM INSTALLED AT THE MYSTIC POWER STATION  OF  THE  BOSTON EDISON
COMPANY CONSISTS OF A CHEMICO-DES1GNED  SINGLE-STAGE VENTUKI SCRUBBER MODULE-   THE MODULE  IS CON-
STRUCTED OF CARBON STEEL LlriEO  WITH A SPRAY-APPLIED POLYESTER MATERIAL.  TOTAL FLUE  GAS CAPACITY OF
THE SYSTEM IS «
-------
BOSTON  EDISON
           BOILER
          OPERATION
MONTH/YR      (HR)
APR.  72
   TO
MAT  73
         SCRUBBER
        OPfcRATION
          (HR)
                   FGO  SYSTEM AVAILABILITY
                                                      MYSTIC  UNIT  NO.  6
        OPERABILITY
             17
JUN. 73
JUL. 73
AUG. 73
SEP. 73
OCT. 73
 NOV. 73
 DEC. 73

 JAN. 74
 FEB. 74

 MAR. 74
 APR. 74
 MAY   74
 JUN.  74
592       402
575       351
   BOILER SHUTDOWN
637       243
627       377
629
658

555
541

408
585
486
559
162
 86

152
138

353
471
280
288
             68
             61

             38
             60
26
li

28
25

87
81
57
80
              THE MODULE  OPERATED  INTERMITTENTLY  BECAUSE UF
              MECHANICAL  DIFFICULTIES.   A  I-AJUR PROBLEM COMCEWN-
              ED THE  OPERATION  OF  THE  MAGNESIUM SULFITE CRYSTALS
              U K T t K 9

              THE LONGEST  PERIOD OF  CONTINUOUS OPERATION, 7.5
              DAYS, OCCURRED  DURING  JUNE  AND  JULY.
              THE BOILER  WAS  DOWN  FOR  THE  ANNUAL  OVERHAUL.
              SYSTEM  AVAILABILITY  DECREASED  DURING  THE LAST
              QUARTER OF  THE  YEAR  BECAUSE  OF  HEAVY  EROSION/
              CORROSION  IN THE  LIQUOR  RECIRCULATION PUMPS AND
              CENTRIFUGE.
SYSTEM AVAILABILITY HAS LIMITED BY BOILER-RELATED
PROBLEMS THAT CAUSED FREQUENT SHUTDOWNS IN JAN-
VARY AND FEBRUARY.

TWO 7-DAY CONTINUOUS OPERATION PERIODS OCCURRED
DURING THE MONTH.

THE 57 PEKCENT OPERABILITY  INDEX VALUE FOR THE
MONTH WAS DUE TO A 2-WEEKS  OUTAGE OF THE ACID
PLANT RATHER THAN TO FGD SYSTEM FAILURE.  DEMON-
STRATION PROGRAM WAS COMPLETED AND FGO SYSTEM WAS
SHUT DOWN.  EPA FUNDING OF  MGS03 CALCINATION HAS
EXPIRED.  THERE ARE NO DEFINITE PLANS FOR RESTART-
ING OF THIS UNIT.  MAJOR PROBLEM AREAS ENCOUNTERED
DURING THE OPERATION OF THIS PROTOTYPE UNIT IN-
CLUDED TRIHYORATE INSTEAD UF HEXAHYDRATE 3ULFITE
CRYSTAL FORMATION, DUST PROBLEMS IN THE DRYER,
LACK OF STACK GAS REHEAT CAUSING CONDENSATION IN
THE STACK, LOUVER DAMPER PROBLEMS, EROSION OF
PUMPS, PIPING, AND CENTRIFUGE, AND MINOR ANCILLARY
EQUIPMENT FAILURES.
                                                   165

-------
                 TABLE 13
DESCRIPTION OF TERMINATED FGD SYSTEMS  01/78
UTILITY NAME

UNIT NAME

UNIT LOCATION

UNIT RATING

FUEL CHARACTERISTICS

FGD VENDOR

PROCESS

NfcW OR RETROFIT

START UP DATE

FSD STATUS

EFFICIENCY,
  PARTICULATES
 CENTRAL  ILLINOIS LIGHT CO.

 DUCK  CREEK  NO.  1A

 CANTON ILLINOIS

  100  MA

 COAL  2.5 -  3.0  PERCENT SULFUR

 RILEY STOKER /  ENVIRONEERING

 LIMESTONE SCRUBBING

 NEW

  9/76

 TERMINATED


 99.8  PERCENT
  S02
                       85  PERCENT
 WATER  MAKE  UP
                       CLOSED  LOOP
 SLUDGE  DISPOSAL
 UNIT  COST
SEE APPENDIX A,  FGO SYSTEM ECONOMICS
 OPERATIONAL
  EXPERIENCE
 THE INSTALLATION OF ONE OF A TOTAL OF FOUR SCRUBBER MODULES WAS
 COMPLETED IN JULY 1976 AND START-OP OPERATIONS COMMENCED. SHAKEDOWN
 AND DEBUGGING OPERATIONS PROCEEDED ON AN INTERMITTENT BASIS
 bECAUSE OF NUMEROUS CHEMICAL AND MECHANICAL-RELATED PROBLEMS.
 THE SINGLt COMPLETED SCRUBBER MODULE HAS BEEN SHUTDOWN UNTIL THE OTHER
 THREE MODULES, hfcpntstNTiNG 300 M« OF SCRUBBING CAPACITY, AHE READY IN
 AUGUST 19/8. UNTIL THAT TIME THE 400-MW UNIT WILL BE UTILIZING COLORADO
 LOW-SULFUR COAL FOR POWER GENERATION OPERATIONS.
                                             166

-------
                                        BACKGROUND  INFORMATION
                                                  ON
                                        DUCK CREtK  PLANT  NO  1A

     THE  DUCK  CREEK PLANT  OF  THE CENTRAL ILLINOIS  LIGHT  COMPANY  (rnrin  ie  .   c
GENERATING  STATION LOCATED IN AN ONRECLAIMEO ST  1P-MIN NG  AREA  NE*J   ANT  N   ILL?M,1 ^''I
PRESENT  TIME,  ONE 400-MW COAL-FIRED UNIT IS IN SERVICE AND  ?HREfc  MORE  IOENHCAL  UNHS  ARE  BM
PLANNED,  BRINGING THE TOTAL  PLANNED PLANT CAPACITY  TO 20OU  Mw.         IDENTICAL  UNITS  ARt  BU

     THE  NO. 1 POWER-GENERATING UNIT INCLUDES A  3-MILLION  L6S./HR.  STEAM-GENERA T IMG  BQIiE
PSIG, 1005F/1005F, SINGLE  REHEAT, PULVERUED-CUAL-FIREO,  BALANCED DRAFT?  SUPPL ED  8Y ?HE
STOKER CORPORATION TO PROVIDE STEAM TO 400-MW TURblNE.   THE BOILER  IS  DESIGNED TO  F  RE hlGH-SULFUR
ILLINOIS  COAL, AVAILABLE FROM NEARBY MINES, HAVING THt FOLLOWING  AVERAGE  CHARACTEKISTICS:   HEAT
CONTENT,  10,500 HTU/Lb;  SULFUR CONTENT 2.4 TO 4.0  PERCENT;  ASH  CONTENT,  6.0 TO 18.U  PERCENT
CONSTRUCTION Of THE NO.  1  UNIT BEGAN IN THE EARLY  PART OF  1972.   COMMERCIAL SERVICE  COMMENCED  IN
JUNE 1976.

     THE DESIGN OF THE  EMISSION CONTROL SYSTEM FOR THIS  UNIT CONSISTS  OF  TWO 99.8  PERCENT-EFFICIENT
ELECTROSTATIC PRECIPITATORS SUPPLIED BY POLLUTION  CONTKOL-WALTHtK (PCw)  FOR THE  COiMTKOL UF
PARTICULATES AND  FOUR WET-LIMESTONE SCRUBBER MODULES  SUPPLIED BY  RILEY STOKEH/ENVIRQNEERlNG  FOK  THE
REMOVAL OF  75 PERCENT OF  THE SULFUR DIOXIDE.  THE  EMISSION CONTROL  SYSTEM IS DESIGNED  TO  FUNCTION  IN
THE FOLLOWING MANNER:   THE BOILER FLUE GAS, AFTER  PASSING  THROUGH TWO  AIR PREHEATER  UNIIS, tNTEHS
THE PCW ESP'S WHERE PRIMARY PARTICULATE REMOVAL  OCCURS.   THt PART ICULAlE-CLEAwEi) GAS IS lriEi<. DIS-
CHARGED TO A MANIFOLD SUPPLYING FOUR CENTRIFUGAL INDUCED DRAFT  FANS (RADICAL TIP,  INLET-DAHPER
CONTROL, 900 RPM,  4000  HP  EACH).  THE FLUE GAS  IS  BOOSTED  THROUGH A COMMON HEADER  INTO THE 
-------
CENTRAL ILLINOIS LIGHT CO.
                                         PERFORMANCE HISTORY
                                               DUCK  CREEK  UNIT  NO.  U
              MODULE
PERIOD     OPERATION HRS.
JOL. 7b       8 HRS.
AUG. 76      18 HKS.
SEP. 7b     360 HRS.
 OCT.  7fa
 NOV.  76
             38i HRS.
                 HRS.
 DEC.  76
 JAN.  77
 FEB.  77
 MAR.  77
             350  HRS.
 APR.  77
 MAY   77
                               COMMENTS
INITIAL OPERATION OF THE FIRST SCRUBBER MODULE FOR SHAKEDOWN  AND  DE-
BUGGING PURPOSE OCCUREU DURING THE MONTH.  LIMITED SEKVICE  TIME  RESULT-
ED FROM PROBLEMS WITH BAD WELDS, FAULTY PIPE HANGES, AND  ABSORBER
LEAKS.

LIMITED OPERATIONS CONTINUED THROUGHOUT AUGUST BECAUSE  OF  THE  START-UP
AND CONSTRUCTION PROBLEMS MENTIONED ABOVE.  THE MODULE  WAS  TAKEN  OUT
OF THE GAS PATH AT THIS POINT TO CONCENTRATE ON RESOLVING  THESE PROBLEM
AREAS.

MODULE RESTART OCCURRED ON SEPT. 9.  OPERATION CONTINUED  THROUGHOUT
THE REMAINDER OF THE MONTH ON AN INTERMITTANT BASIS.  MAJOR PROBLEMS
INCLUDED PIPE BREAKING, PUMP LINER FAILURES, PLUGGING AMD  SEALING OF
MIST ELIMINATORS, AND SOME BOILER-RELATED PROBLEMS.  THE  MODULE RE-
MAlNtD IN SERVICE FOR APPROXIMATELY 15 DAYS OF NON-CONTINUOUS
OPERATION.  THE PCW ESP MODULES HAVE REMAINED IN SEKVICE  WITHOUT  THE
OCCURRENCE OF ANY MAJOR PROBLEMS.

TOTAL OPERATION TIME DURING THE MONTH WAS APPROXIMATELY 16 DAYS
INON-CONTINUOUS).  MAJOR PROBLEM AkEA WAS THE CONTINUATION OF  MASSIVE
SCALE DEVELOPMENT UN THE MIST ELIMINATORS, RESULTING IN PLUGGING  OF
THE PIPING AND NOZZLES TO THE COMPONENTS SPRAY SYSTEM.

SPORADIC OPERATION RESULTED FROM CONTINUED SCALING PROBLEMS IN THE
MIST ELIMINATOR SECTION.  RILEY AND CILCO INITIATED MODIFICATIONS TO
THE DESIGN OF THE MODULE.  SPECIFICALLY, A ROD DECK WAS CHANGED IN THE
ABSORBER, PRESSURE DROP ACROSS THE ABSORBER WAS INCREASED, PIPING AND
PUMP LINER MATERIALS WERE MODIFIED/REPLACED, AND A FRESH WATER WASH
SYSTEM WAS INSTALLED FOR THE MIST ELIMINATOR.

THE MODULE REMAINED OUT OF SERVICE THE ENTIRE MONTH.  DURING THIS
TIME, THE BUILtR FIRED LOW SULFUR (0.6X) KENTUCKY COAL.

THE NO. 1 UNIT WAS DOWN THROUGHOUT THE ENTIRE PERIOD FOR TURBINE/BOILER
OVERHAUL.  DURING THE UNIT OUTAGE, A NUMBER OF MODIFICATIONS WERE MADE
TO THE SCRUBBER.

THE NO. 1 UNIT WAS RETURNED TO SERVICE IN MID-MARCH.  THE SCRUBBER
WAS PLACED IN SERVICE TO TEST THE MODIFICATIONS MADE DURING THE PRE-
CEDING OUTAGE.  THESE MODIFICATIONS INCLUDED:
* THE MIST ELIMINATOR SPRAY WASH SYSTEM PIPING WAS CHANGED FROM PVC
  TO FHP MATERIALS.  ALSO, AN ADDITIONAL SPRAY HEADER WAS ADDED.
  THE SLURRY CIRCULATION SYSTEM WAS REVAMPED.
  NEUPRENE PUMP FILTERS HAVE REPLACED THE ORIGINAL ROBBER LINES.
  FLUSH/DRAIN SYSTEMS HAVE BEEN INCLUDED TO MINIMIZE SOLIDS BUILD UP.
  PIPING VALVES MOVED CLOSER TO THE RECYCLE TANK.
  SLURRY STORAGE TANKS EQUIPPED WI1H FLUSH/DRAIN SYSTEMS.
  ADDITIONAL MIXERS ADDED FOR GREATER AGITATION TO PROMOTE PROCESS
  CHEMISTRY.
DURING THE LAST PART OF MARCH THE MODULE REMAINED IN SERVICE ON A
CONTINUAL BASIS WITH THE EXCEPTION OF A FEW MINOR BOILER OUTAGES.
CILCO INTENDS 10 CONTINUE EXPERIMENTAL OPERATIONS THROUGHOUT THE  APRIL-
MAY PERIOD, TESTING THE MECHANICAL MODIFICATIONS AND THE AUTOMATIC
CONTROL LOOPS (SYSTEM CHEMISTRY WILL BE CONTROLLED 8Y INLET/OUTLET S0£
LOADING,  SOLUTION PH, SOLUTION SOLIDS.  OPERATION UP TO THIS  POINT
HAS PROCEEDED IN A MANUAL CONTROL MODE).  CONTINUED OPERATION  BEYOND
THIS TIME FRAME WILL DEPEND UPON ThE SUCCESS OF EXPERIMENTAL
OPERATIONS.  CILCO HAS THE OPTION OF FIRING LOW SULFUR COAL UNTIL THE
ENTIRE 1-MODULE SCRUBBER PLANT IS READY FOR SERVICE IN AUGUST  1978.

THE UNIT CONTINUED TO HkE LOW-SULFUR COLORADO CUAL DURING THE REPORT
PERIOD.  THE RESTART OF SCRUBBER OPERATIONS CONTINUES TO BE SCHEDULED
FOK AUGUST 1978.
                                                 163

-------
                 TABLE  12
DESCRIPTION OF TERMINATED  FGD  SYSTEMS
                                        01/76
UTILITY NAME


UNIT NAME


UNIT LOCATION


UNIT RATING


FUEL CHARACTERISTICS


F6D VENDOR


PROCESS


NEW OR RETROFIT


START UP DATE


FGD STATUS


EFFICIENCY,
 PARTICULATES
COMMONWEALTH EDISON

WILL COUNTY NO  1

ROMEOVILLE  ILLINOIS

 167 MW

COAL 0.3 PERCENT  SULFUR

BA8COCK & WILCOX

LIMESTONE SCRUBBING

RETROFIT
TERMINATED



98 PERCtNT
  S02
                       82 PERCENT
 WATER MAKE UP
                       OPEN LOOP l.bb GPM/MW
 SLUDGE DISPOSAL
                       HAULAWAY TO LANDFILL
 UNIT COST
                      SEE APPENDIX A, FGD SYSTEM ECONOMICS
 OPERATIONAL
  EXPERIENCE
REFER TU  THE BACKGROUND  INFORMATION SECTION IN TABLE 12 OF THIS REPORT.
THIS FULL  SCALE  DEMONS THAT ION SCRUBBING SYSTEM HAS SEEN IN SERVICE  SINCE
FEBRUARY  1972.  THE  SYSTEM  INCLUDES TWO SCRUBBING 1RAINS FOR THE
CONTROL OF PARTICULATES  AND SULFUR DIUXIDE. MODULE AVAILABILITY,
UPERA8ILITY, RELIABILITY,  AND UTILIZATIUN INDEX VALUES FOR THt REPORT
PERIOD ARE PROVIDED  IN THE BACKGROUND INFORMATION SECTION. EXPERIMENTAL
su2 REMOVAL OPERATIONS WERE CONCLUDED IN JULY i<*77, HOWEVER,  PAKTICULATE
SCRUBBING  OPERATIONS  ARE CONTINUING ON LOH-S WESTERN COAL FLUE GAS.
                                             169

-------
                                       BACKGROUND  INFORMATION
                                                 ON
                                          WILL COUNTY NO.  1

     IN 1970, COMMONWEALTH EDISON CONTRACTED WITH  THE BECHTEL CORPORATION  TO  INVESTIGATE THE SULFUR
REMOVAL SYSTEMS THEN AVAILABLE HAVING A SUFFICIENT DEGREE  OF DEVELOPMENT  TO WARRANT LARGE-SCALE IN-
STALLATION ON WILL COUNTY STATION'S UNIT NO. I.  AFTER DECIDING  ON  A  WET  SCRUBBER  SYSTEM USING LIME
OR LIMESTONE, BECHTEL PREPARED A SPECIFICATION AND RELEASED  IT FOR  BID.   FROM NINE BIDDERS THAT WERE
SOLICITED, SEVEN PROPOSALS WERE RECEIVED.  AFTER DETAILED  STUDY  AND BID EVALUATION WITH SPECIAL CON«
SIDERATION OF THE PROJECT SCHEDULE, BA8COCK AND WILCOX WAS AUTHORIZED IN  SEPTEMBER 1970 TO BEGIN
DETAILED ENGINEERING FOR A LIMESTONE SLURRY SYSTEM.  COMPLETION  DEADLINE  FOR  THE  PROJECT WAS
OECEMbER 31, 1971.  A DEADLINE ESTABLISHED BY THE  ILLINOIS COMMERCE COMMISSION AS  PART  OF A RATE
CASE.

     THE BABCOCK AND WILCOX PROCESS WAS GUARANTEED TO REMOVE 98  PERCENT OF THE FLY ASH  AND 76
PERCENT OF THE SULFUR DIOXIDE.  THESE EFFICIENCIES WERE BASED ON  A  DUST INLET LOADING Of 1.355
GRAINS PER STANDARD CUBIC FOOT AT 70 f AND ON BURNING OF ILLINOIS COAL CONTAINING  4 PERCENT SULFUR.

     THE WILL COUNTY POWER STATION IS LOCATED NEAR ROMEOVILLE, ILLINOIS.   THE PLANT HAS FOUR ELEC-
TRIC POWER GENERATING UNITS WITH A TOTAL RATED CAPACITY OF 1117  MW.   ONLY  UNIT NO. 1  IS RETROFITTED
WITH AN FGD  SYSTEM.

     UNIT NO. 1 IS A WET-BOTTOM COAL-FIRED BOILER  PRODUCING  167  Mrt  OF ELECTRICITY.  THE BOILER WAS
MANUFACTURED BY BABCOCK AND WILCOX AND WAS INSTALLED IN 1S55.  THE  PLANT  NOW  BURNS A  LOW-SULFUR 10.H
PERCENT) WESTERN COAL AND A HIGH-SULFUR (4.0 PERCENT) ILLINOIS COAL.

     THE WET LIMESTONE FGO SYSTEM AT WILL COUNTY WAS PLACED  IN SERVICE ON  FEBRUARY 23,  1972.  THE
SYSTEM CONSISTS OF TWO FGD MODULES (IDENTIFIED AS  A AND B),  LIMESTONE HANDLING AND MILLING FACIL-
ITIES, AND A SLUDGE TREATMENT AND STABILIZATION UNIT.  A PROCESS  FLOW DIAGRAM OF  THE  FGD SYSTEM IS
GIVEN  IN APPENDIX B.  SULFUR DIOXIDE REMOVAL EFFICIENCY HAS  BEEN  MEASURED  AT  82 PERCENT.  SHORTLY
AFTER  STARTUP AND DURING INITIAL SHAKEDOWN, NUMEROUS PROBLEMS WERE  ENCOUNTERED.   COMMONWEALTH EDISON
SHUTDOWN MODULE B IN MAY 1973 TO CONCENTRATE ON SOLVING THE  PROBLEMS  OF MODULE A.   MODULE B WAS NOT
RESTARTED UNTIL MAY 1975.

     THE LIMESTONE GRINDING FACILITIES CONSIST OF  TWO WET  BALL MILLS,  EACH RATED  AT 12  TONS PER HOUR
OF LIMESTONE.  THE LIMESTONE IS 97.5 PERCENT CALCIUM CARBONATE,  AND CONTAINS  0.99  PERCENT MAGNESIUM
CARBONATE AND 0.48 PERCENT SILICA.  IT IS RECEIVED IN COARSE-GROUND FORM  (ABOUT 1/2 INCH OR LESS)
AND FINELY GROUND TO 95 PERCENT THROUGH 320 MESH.

     SLUDGE  FROM THE SYSTEM IS SENT TO A CLARIFIER.  THE OVERFLOW IS  RETURNED TO  THE  PROCESS AND THE
UNDERFLOW IS STABILIZED BY MIXING IT WITH LIME AND FLY ASH.  APPROXIMATELY 200 POUNDS OF LIME AND
400 POUNDS OF FLY ASH ARE USED PER TON OF DRY SuLIDS OF SLUDGE.  THE STABILIZED MATERIAL IS THEN
TRANSPORTED  BY CONCRETE MIXING TRUCKS FOR ULTIMATE DISPOSAL  IN AN OFF-SITE LANDFILL AREA.


PROBLEMS AND SOLUTIONS

1972 - OEMISTER PLUGGING WAS A CONSTANT PROBLEM,   MAINLY BECAUSE  OF HEAVY  LIMESTONE ACCUMULATION ON
THE BOTTOM OF THE DEMISTER AND ALSO BECAUSE OF LOW WASH-WATER PRESSURE CAUSED BY  LEAKS  IN THE POND
RETURN BYPASS.  BECAUSE OF THESE PROBLEMS, MODULES A AND B WERE  OUT OF SERVICE FOR SEVERAL DAYS EACH
MONTH  DURING MARCH, APRIL, JUNE, AND JULY 1972.  THE MODULES WERE ALSO OUT OF SERVICE FROM SEPTEMBER
26 TO  NOVEMBER 21, 1972, BECAUSE THE BOILER WAS DOWN.

     IN ORDER TO SOLVE THE DEMISTER PROBLEM, THE SLURRY NOZZLES  WERE  LOWERED  AND  THE  SLURRY CIRCULA-
TION SYSTEM  WAS LEFT OUT OF SERVICE TO KEEP THE DEMISTER CLEAN.   SINCE THE SITUATION  DID NOT IM-
PROVE, THE OEMISTER ELEMENTS WERE HAND-WASHED.  THIS SOLVED  THE  PROBLEM PARTIALLY, BUT  CAUSED DIFFI-
CULTY  WITH THE VENTUR1 NOZZLES BECAUSE BROKEN ELEMENTS FRUM  THE  DEMISTER  GOT  INTO  THE SLURRY SYSTEM.

     AT HIGH GAS FLOW RATES, THE KEHEATER OF MODULE B VIBRATED EXCESSIVELY.   THEREFORE, MuOULE B WAS
TAKEN  OUT OF SERVICE IN APRIL TU ALLOW REHEATER MODIFICATIONS, WHICH  INCLUDED RE8RACING OF THE RE-
HEATER TUBES AND INSTALLATION OF A BAFFLE PLATE TO REDUCE  THE VIBRATIONS.

     OTHER REASONS FOR OUTAGES WERE EROSION AND PLUGGING OF  SPRAY NOZZLES, INTERNAL AND EXTERNAL
BUILDUP OF DEPOSITS ON VENTuRl NOZZLES, CORROSION, SULF1TE BLINDING PROBLEMS, AND  FAN VIBRATIONS.

     1973 -  OEMISTER PLUGGING CONTINUED.  FURTHERMORE, THE UEMISTfcS ON MODULE B BROKE LOOSE FSOM ITS
MOUNTINGS AND THE RESULTANT CARRYOVER OF WASHWATER PLUGGED THE REHEATER.   THIS REHEATER ALSO LEAKED
BECAUSE OF CHLORIDE PITTING CORROSION.  MODULE A WAS DOWN  FROM APRIL  24 TU MAY 24, 1973, AND MODULE
B REMAINED OUT OF SERVICE FROM MAY 1973 TO MAY dO, 1975.   THERE  WAS NO SCRUBBER OPERATION FROM
AUGUST 27 TO SEPTEMBER 26, 1973.

     IN EFFORTS TO SOLVE THE DEMISTER AND REHEATER PROBLEMS, A CONSTANT UNOERSPRAY AND  INTERMITTENT
OVERSPRAY WERE USED TO WASH ALL THE DEMISTER COMPARTMENTS  UF MODULE A.  EXTRA NOZZLES WERE ADDED AND
A CLEAN WATER SUPPLY WAS MAINTAINED.  THE REHEATER UNIT WAS  ALSU  RETUBED.

     1974 -  ONLY MODULE A OPERATED DURING 1974.  TH£ MAIN  PROBLEMS  WERE FKEEZIMb  UF THE VENTURI
THROAT DRIVE MECHANISM, TANK SCREEN BLINDING, DUCT CORROSION, AND VIBRATIONS.  LOSS OF  BUILDING HEAT
CAUSED EXTENSIVE DAMAGE AND KEPT THE SYSTEM DUWN FOR THE ENTIRE  MONTH OF  JANUARY  1974.

     1975 -  ENTERING 1975 MODULE A WAS OPERATIONAL AND MODULE B  WAS STILL  UNDERGOING MOO IFICATION.
                                                 170

-------
IN THE FIRST  QUARTER OF 1975 THERt  WERE  8  A-MOOULE UUTA&ES,  ONE OF WHICH rtAS A  FORCED  OUTAGE,  DUE  TU
THE  SPLITTING OF A SLURRY HOSE.   MODULE  B  WAS RETURNED TO SERVICE ON MAT id, l<)7b.   THt  UTILITY
BECTOED  TO  OPERATE THE SCRUBBER  ON  ILLINOIS HIGH-SULFUR COAL.  WHEN THIS OPERATION  BEGAN,  A  MULTI-
TUDE OF  PROBLEMS OCCURRED? LOWER PARTICULAU REMOVAL EFF1CIENCItS, HIGH SLURRf  CARRtUvEnS,  OEKlSTER
PLUGGING.  REHEATER COIL FOULING  AND LEAKS.  MODULE A WAS TAKEN OUT OF SERVICE IN MID-JUNE  F0«  T*E
BFMAINDER  OF  1975.  BY MID-SEPTEMBER 19f5 MODULE B WAS TAKEN OUT OF SERVICE OnING TO MASSIVE SCALING
IN THE ABSORBER SYSTEM.   FINALLY, UNIT NO. 1 WAS SHUT DOWN FOR OVERHAUL OF  THE BOILER, TUHSINE,  AND
SCRUBBER IN MID-OCTOBER?  THIS  OUTAGE LASTED MORE THAN H MONTHS.

     PERFORMANCE  FACTORS  FOR EACH MODULE  AND CORRESPONDING COMMENTS FOR THE REPORT  PERIOD ARE P-.E-
SENTED IN THE FOLLOWING  TABLE.
                                                       171

-------
COMMONWEALTH EDISON
                       FGD SYSTEM OPERABILITY   WILL COUNTY  UNIT  NO.  1
PERIOD         OPERA8ILITY  (X)
MONTH/YEAR   MODULE A   MODULE B
MAR. 72          0          35
APR. 72
MAY  72
JUN.
JUL. 72
AUG. 72
 SEP.  72





 OCT.  72




 NOV.  72


 DEC.  72


 JAN.  73

 FEB.  73




 MAR.  73




 APR.  73




 MAY   73

 JUN.  73




 JUL.  73

 AUG.  73


 SEP.  73
                71)
                 79
                            32
                            31
                            21
                            3U
22


 0

22




65
 0

16



51

IS
30


 0

24



11



13



 (I

 0



 0

 0
                            COMMENTS
MODULE A DOWN FOR REPAIR AND MODIFICATION  OF  DEMISTEK WASH PIPING
ASSEMBLY.  MODULE B WAS REMOVED FROM  SERVICE  EVERY 2 OR 3 DAYS TO
HAND-WASH THE OEMI5TER.  OTHER PROBLEMS  WERE  VIBRATION OF REHEAT-
ER TUBE BUNDLE, RAPID EROSION OF SCRUBBER  SPRAY  (MUZZLES, ItPLUGGlNb
OF VENTURI NOZZLES.

MODULE A OUT OF SERVICE FOH 6 DAYS BECAUSE  OF  NEAR-RUPTURE OF A
VENTURI PIPE EXPANSION JOINT AND HEAVY BUILDUP OF  SULlDS  ON DE-
MISTER.  MODULE 6 OUT OF SERVICE MOST OF THE  TIME  FOR SIMILAR RE-
PAIR OK VENTURI PIPE EXPANSION JOINT, AND  FUR  MODIFICATION OF RE-
HEATER UNIT ANO OEMISTER WASH SYSTEM.

A TWO-WEEK OUTAGE OF MODULE B WAS INCURRED  TO  REBRACE THE REHEAT-
ER UNIT, INSTALL UNDERSPRAY NOZZLES ON DEMISTER, AMD INSTALL  HEA-
VIER SCREENS IN THE SUMP.  RtHEATEH PLUGGING  CAUSED  ADDITIONAL
OUTAGES.

BOTH MODULES WERE OUT OF SERVICE OWING TO  HIGH DIFFERENTIAL PRES-
SURE ACROSS THE DEMISTERS.  LEAKAGE OF A POND  RETURN BYPASS VALVE
CAUSED DtMISIER PLUGGING.  ALSO DURING THIS PERIOD,  THE RUBBER
LINING IN MODULE A WAS REPLACED

PLUGGING OF VENTURI NOZZLES AND DEMISTER CAUSED  SHUTDOWN  OF MOD-
ULE A FOR 2 DAYS FOR REPAIRS.  MODULE B WAS OUT  OF SERVICE FOR 22
DAYS FOR CLEANING OF THE DEMISTER ANO REHEATER UNIT,  INSTALLA-
TION OF OVERHEAD SPRAY NOZZLES AND REPLACEMENT OF  SECTIONS OF THE
OEMISTER.  THE UNIT WAS SHUT DOWN FOR TWO  DAYS FOR TURBINE-GENER-
ATOR REPAIR.

BOILER DOWN SEPT. 1-b BECAUSE OF NO DEMAND.   1.0.  FAN PROBLEM
CAUSED UNSIABLE OPERATION OF THE BOILER MOST  OF  THE  MONTH.
MODULE A WAS DOWN FOR MODIFICATION OF REHEATER UNIT  AND REPAIR OF
RECIRCULAT10N TANK SCREENS.

BOILER AND SCRUBBERS WERE DOWN.  PRINCIPAL MODIFICATIONS  INCLUD-
ED INSTALLATION OF REHEATEH BAFFLE PLATES  TO  DAMPEN  VIBRATIONS
AND INSTALLATION OF AN EXPERIMENTAL OEMISTER  WASH  SYSTEM.

BOILER PROBLEMS CAOS1NG UNSTABLE OPERATION KEPT  BOTH  MODULES  DOWN
DURING THIS MONTH.

MODULES OPERATED INTERMITTENTLY BECAUSE OF ELECTROSTATIC  PRECIP-
ITATOR TESTING AND MISCELLANEOUS INSTRUMENT PROBLEMS.

BOTH MODULES WERE DOWN FUR REPAIRS AND MODIFICATIONS.

MODULES WERE OUT OF SERVICE BECAUSE OF CRACKS  IN THE  INLET DUCT-
WORK OF THE BOOSTER FAN.  IMPROPER INSTALLATION  OF THE  DEMISTER
IN THE B-SIDE CAUSED KEHEATER PLUGGING.

MODULE A WAS OUT OF SERVICE FOR 5 DAYS BECAUSE OF  DEMISTER PLUG-
GING.  BDILER WAS DOWN FOR 4 DAYS OF  INSPECTION.   MODULE  B WAS
OOwN BECAUSE OF LEAKS FROM REHEATER TUBES.

PERSISTING PROBLEMS WITH DEMISTER AND DEPOSITS OF  CALCIUM  SULFATE
SCALE ON REHEATER TUBES OF MODULE A WERE ENCOUNTERED  DURING Trit
MONTH.

BOTH MODULES WERE OUT OF SERVICE DURING  THIS  MONTH.

MODULE B WAS KEPT DOWN TO ALLOW CONCENTRATION  ON THE  PROBLEMS
WITH MODULE A.  BOILER-RELATED PROBLEMS WERE  RESPONSIBLE  FOR  MOST
OF THE OUTAGES OF MODULE A.

MODULE A PROBLEMS:  REHEATER TUBE LEAKS AND HIGH FAN VIBRATIONS.

MORE REHEATER TUBE LEAKS ON MODULE A  ATTRIBUTED  TO CHLORIDE CON-
ROSION ATTACK.

MODULES WERE DOWN.  DURING THIS MONTH CHICAGO  FLY  ASH CO.  FINISH-
ED CLEANING AND TREATING THE NORTHEAST HALF OF THE SLUDGE POND.
                                                 172

-------
COMMONWEALTH EDISON

PERIOD         DURABILITY  (X)
MONTH/YEAR   MODULE  A    MODULE B

OCT. 73         id           0
                                        FGD SYSTEM OPEKA8ILITY    *ILL  COUNTY  UNIT  NO.  1

                                                                  COMMENTS
NOV.  73




DEC.  73




JAN.  7tt




FEB.  74




MAR.  71


APR.  7a





MAY  71


JUN.  IH



JUL.  74




AUG.  74




SEP.  74




OCT.  74


NOV.  74



DEC.  74


JAN.  75


FEB.  75
                51
                 21
                 72
                 93
                 55
                 91
                 94
                 97
                 99
                 99
                99
                   °F HODUU  *  R"EAUD  SOME  PLUGGING.   MODULE
  Ri,Tin      » °  CLEANING  AND  SOME  MOO IF 1C A T ION .   POUR  GAS  DIST-
RIBUTION  IN MODULE SUSPECTED  To CONTRIBUTE  TO OEMISTER PROBLEMS.

MODULES WERE DOWN.   THE  MONTH WAS  DEVOTED  TO  MODIFICATION  AND
ISOLATION"! PARTICULARLr "MISTER,  VENTURI  THROATS,  PUMPS,  ANO


MODULES WERE DOWN OWING  TO  FREEZING  IN  THE  1 U-INCH-0 1 AME TErt ,  4400
FT. LINE  BETWEEN MODULES AND  POND.   SOME  DAMAGE  TO  SUMP  PUMPS OC-
CURRED.   FREEZING ALSO DAMAGED  SOME  INSTRUMENTS.

THE FROZEN PIPELINE  WAS  THAWED,  REANCHURED,  AND  WETUKNED  TO  SER-
VICE.  THE INSTRUMENTS DAMAGED  BY  FREEZING  WERE  KEPA1RED.   MODULE
A WAS KEPT DOWN UNTIL ARRIVAL OF  SECOND-STAGE DEMlSTER.

MODULE A  HAS READY FOR SERVICE  MARCH 20  BUT  HAS  NOT  RETURNED  TO
SERVICE TILL MARCH 27 BECAUSE THE  BOILER  WAS  DOWN.

MODULE A  CONTINUED TO OPERATE UNTIL  APRIL  19  (EXCEPT  FOR  TWO
SHORT INSPECTION OUTAGES) FOR 23  CONSECUTIVE  DAYS.   OPERATION WAS
ON LOW-SULFUR COAL.  SUMP SCREEN  FROM MODULE  B WAS  SUBSTITUTED
FOR DAMAGED SCREEN IN MODULE  A.

MODULE A  OPERATED FUR ENTIRE  MONTH  EXCEPT  FOH SHORT  OUTAGES  FOH
INSPECTION.  MUCH OF THIS OPERATION  WAS  ON  HIGH-SULFUR COAL.

MODULE A  OPERATED FOH ABOUT  iOO HOURS.   THE  SYSTEM  WAS OFF  FOR 2
WEEKS FOR REPAIR OF  VENTURI  THROAT  DRIVE.

MODULE A  OPERATED FOH THE ENT IKE  MUNTH  EXCEPT FOR  AN  INSPECTION
OUTAGE AND TwO BOILER SHUTDOWNS.   MODULE  8  WILL  REMAIN DOWN  UN-
TIL SATISFACTORY OPERATION  OF MODULE A  is  ACHIEVED.

MODULE A  WAS DOWN SIX TIMES  THIS  MONTH;  1HKEE TIMES  BECAUSE  OF NU
BOILER DEMAND, TWICE FOR REPAIK OF  LEAKS  IN  STEAM  PIPING,  AND
ONCE FOR  BALANCING OF A  FAN.

MODULE A  WAS OFF THREE TIMES; ONCE  FOR  CLEANING  UF  DEPOSITS  FKUM
THE VENTURI 1HKOAT,  ONCE FOR  REPAIR  OF  A  DESUPERHEA TER LEAK,  AND
ONCE BECAUSE BOILER  WAS  DOWN.

MODULE A  WAS DOWN FOUR TIMES; ONCE  BECAUSE  OF BOILER  OUTAGES,
ONCE FOR  INSPECTION, AND TwICE  FOR  HEPAIR  UF  HEHEATEK LEAKS.

MODULE A  WAS OUT OF  SERVICE  THREE  TIMES;  TwICE BECAUSE OF  llO DE-
MAND AND  ONCE FOR INSPECTION.

MODULE A  WAS DOWN TWICE; ONCb FOR  INSPECTION  AND ONCE FOK REPA1H
OF VALVE  IN SPENT LIQUOR LINE TO  POND.

MODULE A  WAS DOWN TWICE; ONCE FOR  INSPECTION  AND ONCt FOR NO DE-
MAND.  MODIFICATION  OF MODULE B IS  CONTINUING.

MODULE A  WAS OUT OF  SERVICE  TWICE;  ONCE  FUR  INSPECTION  AND ONCt
FOR NO DEMAND.  ONE  SMALL REHEATER  LEAK  IN A  STAINLESS  STEEL BUN-
DLE WAS BLANKEO-OFF  UN-LINE.  DURING THE  INSPECTION DEMISTEH UN-
DFRWASH NOZZLES WERE CLEANED  AND  A  SMALL  SECTION OF  OtMISTER WAS
HFPLACED   INSPECTION SHOWED  THAT  CONDITIONS  INSIDE THE  SCRUBBER
WERE ABOUT THE SAME  AS BEFORE.   COAL BURNED  THIS MONTH  AVERAGED
TeSS THAN IX SULFUR.  MODIFICATION  OF MODULE  B IS CONTINUING.
CHICAGO FLYASH IS TREATING  MATERIAL  FRUM  THE  SCROBdER WITH PORT-
LAND CEMENT AND FLYASH AND  DUMPING  THE  TXEAUD MATERIAL  INTU THE
NORTH HALF OF THE HOLDING 8ASIN.
                                                  173

-------
COMMONWEALTH EDISON                                              WILL COUNTY UNIT NO. 1

                                 SYSTEM  PERFORMANCE  FACTORS (X)
PERIOD     MODULE     AVAILABILITY   OPERABILITY   RELIABILITY   UTILIZATION
MONTH/YEAR

MAR. 75      A             94             99            93            81
       MODULE A WAS DOWN FOUR  TIMES;  TWICE FOR  NO DEMAND,  ONCE  FOR A VENTURI HOSE LEAK, ONCE FOR AN
       ACCIDENTAL 50-MINUTE  TRIP.   THE  SYSTEM OPERATED ON  LOW SULFUR COAL DURING THE MONTH.  MODULE
       6 MODIFICATIONS  ARE CONTINUING.

APR. 75
             A             37             40            36            35
       SLUDGE POND WAS  OVERBURDENED  BY  NEAR-CONTINUOUS OPERATION OF MODULE A.  THE FSD SYSTEM WAS
       SHUT DOWN  TO ALLOW EVAPORATION OF  WATER  FROM THE PONO.  DURING  SHUT-DOWN THE FOLLOWING MODI-
       FICATIONS  WERE MADE:  PUMP  GLAND WATER FLOWS WERE  REDUCED FROM  10 TO 5 GPM (FILTER BACKWASH
       WAS ROUTED OUT OF SYSTEM),  CONTINUOUS DEMISTER  UNDERSPRAY WAS CHANGEO TO INTERMITTENT.  RE-
       CLAIM COAL WAS BURNED IN  THE  BOILER DURING THE  MONTH.

MAY  75      A             64             84            84            64
             B             37             37            37            37
       MODULE A REMAINED OUT OF  SERVICE UNTIL MAY 5 WHEN  IT  WAS DETERMINED THAT THERE WAS ENOUGH
       FREEBOARD  IN THE POND TO  START OPERATING.  THERE WERE  TWO MORE  OUTAGES;  ONE FOR 45 MINUTES,
       THE RESULT OF A  DAMPER  TRIP,  THE OTHER FOR CLEANING OF UNDERSPRAY NOZZLES.  MODULE B WAS
       PLACED IN  SERVICE AT  TEN  A.M.  MAY  SO FOR  THE FIRST  TIME  SINCE NOON ON APRIL 13,  1973.  AFTER
       bRIEF START UP,  WHICH WAS ROUTINE, OPERATION WAS DELAYED UNTIL  THE 20TH  BECAUSE OF TwO BRO-
       KEN OIL PUMPS UN THE  RECIRCULATION TANK  MIXERS. SINCE THE STARTUP MODULE 8 HAS BEEN OUT OF
       SERVICE IWICE; ONCE FUK A VENTURI  PUMP TRIP  AND ONCE  FOR A RECIRCULATION TANK LEVEL TRIP.
       THE TOTAL  OUTAGE TIME WAS ONLY 1 HOUR, 40  MINUTES.   RECLAIM COAL OF VARYING SULFUR CONTENT
       WAS AGAIN  BURNED IN THE BOILER.  THE SCRUBBER SLUDGE  WAS STABILIZED WITH LIME AND FLYASH AND
       STORED IN  THE HOLDING BASIN.

JUN. 75      A             64             61            60            54
             B             85             85            84            75
       MODULE A SUSTAINED FIVE OUTAGES  DURING THE MONTH.   THE MODULE IS PRESENTLY OUT OF SERVICE TO
       ALLOW INSTALLATION OF NEW DEMISTERS AND  REHEATERS.   MODULE 3 WAS OUT OF  SERVICE  EIGHT TIMES.
       LONGEST OUTAGE WAS 95 HOURS  FOR  CLEANING  OF  BOOSTER FAN  AND DEMISTER.  BOOSTER FAN VIBRATIONS
       CAUSED A SHUTDOWN ON  JUNE 30.  A HIGH SULFUR COAL  TEST BURN WAS CONDUCTED FOR APPROXIMATELY  I
       WEEKS.  LOW SULFUR WESTERN  COAL  WAS BURNED IN THE  UNIT FOR THE  REMAINDER OF THE  MONTH.

JUL. 75      B             79             79            77            74
       MODULE A CANNOT  BE RETURNED  TO SERVICE UNTIL THE NEW  REHEATER ORDERED IN APRIL IS RECIEVED
       AND  INSTALLED.   MODULE  8  SUSTAINED FOUR  OUTAGES, ONE  FOR NO DEMAND.  REHEATER FAILURES AT
       1000 HOURS SEEM  TO BE CAUSED  BY  VIBRATION  FATIGUE.   ONE  MINOR STEAM HEADER LEAK  ALSO OCCUR-
       RED.  LOW  SULFUR COAL WAS bURNED DURING  THE  FIRST  3 WEEKS AND HIGH SULFUR ILLINOIS COAL  WAS
       BURNED DURING THE LAST  WEEK  OF THE MONTH.

AUG. 75      B             94            100            92            76
       MODULE A REMAINED OUT OF  SERVICE ALL MONTH.   MODULE B  WAS SHUT  DOWN SEVEN TIMES  DURING THE
       MONTH, FOUR OF WHICH  WERE DUE  10 "NO DEMAND."  HIGH SULFUR PILE COAL WAS BURNED  IN TnE UNIT
       DURING THE MONTH, RESULTING  IN A SUBSTANTIAL INCREASE  IN SLUDGE PRODUCTION AND FORCING A
       6-DAY, 10  HR/DAY, SLUDGE  DISPOSAL  OPERATION. SLUDGE  STABILIZATION IS CONTINUING.

SEP. 75      B             63             63            63            63
       MODULE A REMAINED OUT OF  SERVICE ALL MONTH BECAUSE  OF  DELAY ON  THE NEW REHEATER  ORDER.
       MODULE 8 WAS DOWN 8 TIMES BECAUSE  OF MASSIVE ABSORBER  SCALE, OEMISTEH AND 1.0. BOOSTER FAN
       CLEANING,  BALANCING 1,0.  BOOSTER FAN, AND  PLUGGING  OF  ABSORBER  PUMP SCREEN.  TOTAL OUTAGE
       TIME WAS 236 HOURS, 40  MINUTES FOR CLEANOUT  AND FAN BALANCING.   HIGH SULFUR COAL WAS BURNED
       IN  THE BOILER WHEN THE  SCRUBBER  WAS IN THE GAS  PATH.

OCT. 75      B             32           100            2b            26
       ON  OCTOBER 11, OVERHAUL BEGAN  ON THE WILL  COUNTY UNIT  NO. 1 BOILER, TURBINE,  AND SCRUBBER.
       MODULE 6 EXPERIENCED  TWO  MINOR OUTAGES DURING THE  11-DAY PERIOD PRIOR TO THE OVERHAUL.
       MODULE A REMAINED OUT OF  SERVICE PENDING  DELIVERY  OF  THE NEW REHEATER.

NOV. 75            TURBINE, BOILER,  AND  SCRUBBER  OVERHAUL
       THE SCHEDULED OVERHAUL  OF THE  BOILER, TURBINE,  AND  SCRUBBER MODULES CONTINUED.  MAJOR
       MAINTENANCE AREAS INCLUDED  MODULE  REHEATERS, PONO  RETURN PUMP,  VENTURI SPRAY NOZZLES, VENTURI
       AND ABSORBER MODULES, PUMP  VALVES, AND SUMPS.

DEC. 75            TURBINE, BOILER,  AND  SCRUBBER  OVERHAUL
       MODULE B REHEATER WAS RETURNED FROM MANUFACTURER AFTER REPAIRS  AND REVISIONS.  SCRUBBER
       REHEATERS  COULD  BE INSTALLED  AND OPERATING BY THE  END  OF JANUARY.

JAN. 76            TURBINE, BOILER,  AND  SCRUBBER  OVERHAUL
                                                  174

-------
COMMONWEALTH EDISON
                                                                  WILL  COUNTY  UNIT  NO.  1
                                 SYSTEM PERFORMANCE  FACTORS  fil
                                     UPERABILm   RELIABILITY* ' UT ILIZ A , ION
FEB.  76           TURBINE,  BOILER,  ANU SCRUBBER  OVERHAUL
       THE UNIT REMAINED  UUT  OF SERVICE FOR COMPLETION  OF  THF
       THAT BEGAN ON OCTOBER  U.  1975.  SYSTEM KE»!1S?  IS
MAR. 76
                            30
                                          45
                                                        21
                                                         8
                                                                     iq
       REMAINED AVAILABLE  FOR SERVICE T«E REST  OF  TH

                                                                T  E
                                                                                    '  TU""NE  "°
49
                                                              OF
APR. 76      A              £3           gy
             fc>              51           49
           A & ri*                        2u
       DURING THE MONTH  OF  APRIL THt A-SIDE  INCURRED  PUMP  LINER  FAILURES  WHEN  AN  ISOLATION
       BROKfc AND FELL  INTO  IHt VENTUR1 KtCYCLE  PUMP.   fl-StOE  OUTAGES  DURING  APRIL  HtSoLTEU  FKOM
       REHEATER TUBE BUNDLE LEAKS, PLUGGED ABSUkBtR  TANK SCREEN,  AND  VENTURI PUMP  LINE  FAILURE
       HIGH SULFER  COAL  (3.5 PERCENT SULFUR) HAS  BURNED  IN THE UOILER THROUGHOUT  THt  MONTH    IN
       ADDITION, THE UTILITY INITIATED A TESTING  AND  EVALUATION  PROGRAM OORING  THE  MONTH.   THIS
       PROGRAM IS DESIGNED  TO PROVIDE DATA AND  INFORMATION CONCERNING CHEMISTRY AND RELATED
       OPERATING CHARACTERISTICS.

MAY  76      B              B7            bb            8b            76
       THE A-SIDE WAS  DOWN  THE ENTIRE MONTH  AWAITING  A PARTS  SHIPMENT (VENTURI  PUMP LINERS).  MUDOLE
       B ENCOUNTERED FOOR  FURCED SCRUBBER OUTAGES.   THREE  OF  THESE  OUTAGES WERE MECHANICAL  PROBLEMS,
       DUE TO A VENTURI  HOSE LEAK, PLUGGED ABSORBER  TANK SCREEN,  AND  A FOOLED  I.D.  BOOSTER  FAN.
       HIGH SULFER  ILLINOIS COAL WAS BURNED  IN  \ HE BOILER  DURING  THE  MONTH.  THE  SLUDGE HAS
       STABILIZED WITH LIME AND FLY ASH AND  HAULED TO  AN OFF-SITE DISPOSAL AREA.

JUN. 76      A              bO            44            42            3b
             B              63            6b            81            70
           A & B*                         37                         31
       SIDE-A WAS RETURNED  TO SERVICE JUNE 9 FOLLOWING THE INSTALLATION OF A NErt  VENTURI PUMP LINE«.
       FOUR  FORCED SCRUBBER OUTAGES WERE REPORTED TWO BECAUSE OF NO  DEMAND, ONE  FUR  A  BYPASS DAMPER
       FAILURE AND  ONE FOR  1.0. BOOSTER FAN  FOULING.   THE  B-SIDE  ENCOUNTERED SEVERAL  FORCED SCRUBbER
       OUTAGES, TWO DUE  TO  NO DEMAND AND SEVERAL  SHORT TRIPS  BECAUSE  UF SCALING AND PLUGGING  IN THt
       VENTURI TANK SCREEN.  HIGH SULFUR ILLINOIS COAL WAS BURNED IN  THE  SUILER DURING  IHt  MONTH.
       SLUDGE FIXATION AND  HAULAWAY TO A DISPOSAL SITE CONTINUED.

JUL. 76      A              ^0             0            0            0
             B              86             "JO           84            72
       THE A-SIDE REMAINED  UUT OF SERVICE THE ENTIRE  MONTH BECAUSE  OF  REPAIRS  TO  A  DAMAGED  ABSORBER
       PUMP AND POND THICKENER SLUDGE OVERLOADING.   THE B-SIDE ENCOUNTERED FOUR FORCED  SCRUBBER
       OUTAGES, TWICE  FUR  NO DEMAND, ONCE TD BALANCE  THE I.D. BOOSTER FANS,  AND ONCE  TO WASH  THE
       I.D. BOOSTER FANS.

AUG. 76      A              98           57             96            38
             B              65           61            54           41
           A & B*                        17                        11
       THE A-SIDE REMAINED  UUT UF SERVICE 50 PERCENT  OF THE TIME  DURING THE  MONTH  TO  AVOID  POND
       THICKENER OVERLOADING.  FOUR SCRUBBER OUTAGES  WERE  REPORTED, ONE BECAUSE OF  NO DEMAND  AND
       THREE BECAUSE OF  MINOR PROBLEMS.  THE 8-SIDE ENCOUNTERED  THREE  NO-DEMAND OUTAGES, Two  BECAUSE
       OF LOSS OF CHEMICAL  CONTROL, ONCE FOR FOULING  AND ONCE FOR SPENT SLURRY  VALVE  REPAIRS.
       EXPERIMENTATION WITH THE SYSTEM'S PROCESS  CHEMISTRY, BY LOwEKlNG THE  PH  SET  POINT FROM 5.4 TU
       b.l, WAS CONDUCTED  BY THE UTILITY DURING THIS  PERIOD.  THIb  VARIATION IN OPERATION WAS
       BELIEVED TO  HAVE  CAUSED THE MASSIVE GYPSUM SCALING  IN  B01H MODULES WHICH OCCURRED DURING THE
       PER 100.  THE PH SET  POINT WAS RETURNED BACK TO  THE  5.4 VALVE.   HIGH SULFtR  ILLINOIS  COAL WAS
       BURNED IN THE BOILER DURING THE MONTH.   SLUDGE  STABILISATION PRACTICES CONTINUED.
 SEP. 76
42
79
29
76
28
74
                                                                    60
                         sr;
           •
                                                  1 75

-------
 COMMONWEALTH EDISON


 PERIOD    MODULE

MONTH/YEAR

OCT. 76
NOV. 7fa
                                SYSTEM PERFORMANCE FACTORS  (X)

                      AVAILABILITY  OPERABILITY  RELIABILITY   UTILIZATION
                                                                 WILL  COUNTY  UNIT NO. 1
                           30
                           76
                            0
                                          29
                                          56
                                           0
26
70
 0
28
55
 0
             A             20            26           20            20
             6             72            70           66            55
           A & b*                         8                          1
       PROBLEMS RELATED TO THE A-SIDE SCRUBBER WERE DUE PRIMARILY  TO REPAIRS  NECESSARY TO THE 1A1
       RECYCLE PUMP,  AND DELAYS IN KEPLACEMtNT PARTS SHIPMENTS.   THE A-SIDE MODULE  WAS IN SERVICE
       WHEN THE 8-SIOt WAS DOWN,  HOWEVER SCRUBBING LIJUOR FLOW WAS  REDUCED BECAUSE  ONLY ONE RECYCLE
       PUMP WAS IN USE.  AT THE END OF NOVEMBER, THE REMAINING A-SIDE  PUMP WAS  TAKEN OUT  OF SERVICE
       FOR UVERHAUL ANU REPAIRS.   FOLLOWING THIS THE A-SIDE WILL  RESUME  OPERATIONS  ON ONE PUMP.   ON
       THE B-SIDE, 3 FORCED SCRUBBER OU1AGES OCCURRED DURING OCTOBER.  ONE WAS  BECAUSE OF REPAIRS
       OF A REHEATER HEADER LEAK  AND THE TIE-IN OF A VACUUM FILTER  AT  THE  THICKENER.  THE OTHER  TWO
       RESULTED FROM A VENlORI NOZZLE CLEAN-OUT AND A VENTORI LOW-FLOW TRIP.  DURING NOVEMBER, 4
       SCRUBBER TRIPS OCCURRED BECAUSE OF A MILLING SYSTEM FAILURE,  VENTURI HEADER  LEAK REPAIR AND
       VENTURI NOZZLE CLEANING, REPLACEMENT OF SPENT SLURRY VALVE,  AND CHEMICAL SYS1EM UP3ET.  TWU
       OUTAGES WERE ALSO LOGGED BECAUSE OF NO DEMAND.
       *NOTE- A&B DESIGNATION AND THE CORRESPONDING PERFORMANCE VALUES REFER  TO THE  SIMULTANEOUS
              OPERATION OF BOTH SCRUBBING TRAINS DURING THE REPORT  PERIOD  IN  UUEST10N.

DEC. 76      A             45            46           45            45
             B             53            52           51            48
       THE A-SIDE WAS PLACED IN SERVICE DURING THE LATTER PART OF  THE  MONTH AND OPERATED  CONTINUOSLY
       WITH THE EXCEPTION OF ONE  MINOR OUTAGE FOR SLURRY VALVE REPAIRS.  A SPENT SLURRY VALVE
       FAILURE FORCED THE 8-SIDE  OUT OF SERVICE THE REMAINDER OF  THE MONTH.   SIMULTANEOUS MODULE
       OPERATION TIME WAS 0 HOURS.  THE SCRUBBER MODULES ARE SEEING  SERVICE ON  A ROTATIONAL BASIS,
       I.E., ONE MODULE UP. ONE MODULE DOWN.  SLODGE STABILIZATION  PRACTICES  AND OPERATION ON LOW
       SULFUR COAL CONTINUED DURING THE MONTH.

JAN. 77      A             98            99           9H            96
             B             14             111
       ROTATIONAL MODULE OPERATIONS CONTINUED.  A-SIDE OUTAGES WERE  SPENT  SLURRY VALVE FAILURE
       AND PLUGGED DEMISTER UNDERSPRAYS.  THE DECEMBER SPENT SLURRY  VALVE  FAILURE KEPT THE B-SIDE
       OUT OF SERVICE UNTIL JAN.  27.  ACTOAL B-SIOE SERVICE TIME  WAS ONE DAY.   SLUDGE STABILIZATION
       AND DISPOSAL PRACTICES CONTINUED.  LOW SULFUR WESTERN COAL  WAS  BURNED  IN THE  BUILER.  SIM-
       ULTANEOUS MODULE OPERATION WAS 0 HOURS.

FEB. 77      A             39            42           39            39
             B             72            45           60            41
           A&B*                        13                         12
       DURING THE ENTIRE MONTH OF FEB. 1977, LOw-SULFUR COAL WAb  BURNED  IN THE  BOILER.  THERE WAS
       VERY LITTLE DIGGING IN THE REC IRCUL AT I ON PONDS.  CHICAGO FLYASH SPENT  MOST OF THEIR TIME  ON
       CLEANING AND MAINTENANCE.   MODULE A WAS OFF THE FIRST PART  OF THE MONTH  FOR  CLEANING OF ON-
       DERSPRAYS, OVERSPRAYS AND  ABSORBER SPRAY NUZZELS.  PLUGGING  WAS CAUSED BY A  FAILED CLASSIFIER
       LINER, WHICH ALLOWED OVERSIZED PARTICLES TO ENTER THE SYSTEM.   THE  CLASSIFIER LINER WAS RE-
       PLACED.  MODULE B WAS FORCED OUT OF THE GAS PATH THREE TIMES  THIS MONTH.  THE REASONS HERE:
       HIGH VIBRATION OF I.D. BOOSTER FAN,  REPACKING OF 1B1 AND  182 ABSORBER PUMPS, AND  BEARING
       FAILURES IN A AND 8 SLURRY TRANSFER PUMPS.

MAR. 77      A             97            66           95            b4
             B             HI            75           79            73
           A&B*                        52                         51
       IN MARCH AN ERT S02 ANALYZER WAS INSTALLED ON THE DISCHARGE  SIDE  OF B  MODULE  I.D.  BOOSTER
       FAN.  THIS IS AN "IN SITU" NON-DISPERSIVE ANALYZER THAT CONTINUALLY MEASURES  AND MEADS OUT
       CONCENTRATIONS OF S02, CU2, CO AND NO.  HIGH-SULFUR COAL WAS  BURNED FOR  SEVEN DAYS DURING
       MARCH TO PROVIDE HIGH SOLFUR SLUDGE FOR THE U.O.P.  SLUDGE  TEST IA  U.O.P. TEST CREW WAS
       EXPERIMENTING WITH POWERTON FLYASH AND HIGH-SULFUR SLUDGE).   CHICAGO FLYASH  SPENT  ABOUT 75%
       OF THEIR TIME DIGGING IN THE RECIRCUL A T ION PONO.  THE REST  WAS  SPENT ON  THE  THICKENER AND
       VACUUM FILTER OPERATIONS.   THE SCRUBBER WASTE MATERIAL WAS  TREATED  WITH  LIME  AND FLYASH AND
       HAULED TO AN OFF-SITE DISPOSAL AREA.  MODULE FORCED OUT OF  THE  SAS  PATH  ONCE  THIS  MONTH TO
       ALLOW FOR REPAIR TO A VENTURI FLOW DIFFERENTIAL LINE.  MODULE FORCED OUT OF  THE GAS PATH  FOUR
       TIMES.  THE REASONS WERE:  REPTUftED DIAPHRAM ON REHEATEK STEAM VALVE, ABSORBER SUCTION LEAK,
       SPENT SLURRY VALVE GASKET  LEAK AND PLUGGED FEED SLURRY KEC IHCULAT ION LINE.
                                                 176

-------
COMMONWEALTH  EDISON
 PERIOD     MODULE
MONTH/YEAR
                                                                WILL COUNTY UNIT NO. 1
                      AVA1I4RI,in  PERFORM*NCE FACTORS U)
                      AVAILABILITY  OPERABILITY  RELIABILITY  UTILIZATION
APR.  T7
             A
             B
             &  B*
                           86
                           45
       RPKN

                           68           61           61
                           30           33           21

                  « THE A'8IOE DUR1NG APRIL- ONE FOR°A 8oii-ER TU8E LEA* REPAIR« AND
                 InROAT LEAK>  B'SIOE OUTAGES OCCURRED TWICE FOR ABSORBER SUCTION
                 !°.r*8H THE I
-------
COMMONWEALTH                                                    WILL COUNTY  UNIT  NO.  1

                                 SYSTEM PERFORMANCE FACTORS  (X)
 PERIOD    MODULE     AVAILABILITY  OPERABILITY  RELIABILITY  UTILIZATION
MONTH/YEAR

OCT. 77           TURBINE/ BOILER AND SCRUBBER OVERHAUL

NOV. 77      A              0             0            0            0
             B              9            50            9            9
       UNIT 1 CAME ON LINE FOLLOWING A SIXTY-THREE DAY UNIT OUTAGE ON 11/25/77.   A MODULE, HOWEVER,
       WAS STILL UNDERGOING SUMP REPAIRS WITH AN EXPECTED SERVICE DATE OF LATE DECEMBER.  B MODULE
       IS IN GAS PATH AFTER EXPERIENCING SOME DIFFICULTY IN BALANCING ITS BOOSTER FAN.

DEC. 77      A             43            48           43           42
             B             84            94           84           84
       THE MONTH OF DECEMBER SAW TROUBLESOME REHEAT PLUGGING ON B MODULE.  BECAUSE OF NO SPARE
       REHEAT-COILS WE TRIED TAKING SOME COILS FROM A MODULE TO USE IN B MODULE;  HOWEVER, B MODULE
       SEEMS TO BE PLUGGED MORE SEVERELY THAN ORIGINALLY BELIEVED.  A MODULE WAS  DOWN HALF THE
       MONTH BECAUSE OF A MAIN STEAM LEAK WHICH COULD NOT BE ISOLATED AND FINISHING THE DAMAGED
       SUMP FLOOR.
       CHICAGO ADMIXTURES SPENT MOST OF THEIR TIME OPERATING OUT OF THE THICKENER.  THE WASTE MATER-
       IAL WAS TREATED WITH LIME AND FLYASH AND HAULED TO A DISPOSAL AREA.
                                                178

-------
                 TABLE 12
DESCRIPTION OF TERMINATED F6D SYSTEMS   01/76
UTILITY NAME          DAIRYLAND POWER COOP

UNIT NAME             ALMA STATION

UNIT LOCATION         ALMA WISCONSIN

UNIT RATING             60 MM

FUEL CHARACTERISTICS  COAL   3.0-3.5 PERCENT  SULFUR

FGO VENDOR            FOSTER WHEELER

PROCESS               LIME INJECTION

NEW OR RETROFIT       RETROFIT

START UP DATE          6/71

F60 STATUS            TERMINATED

EFFICIENCY.
 PARTICULATES


 S02                  25 PERCENT


WATER MAKE UP


SLUDGE DISPOSAL


UNIT COST


OPERATIONAL           THIS EXPERIMENTAL  WET LIME  FURNACE  SYSTEM  BEGAN  OPERATIONS  IN  '71  AND  WAS
 EXPERIENCE           OPERATIONAL  FOR PERIODS UP  TO  30  DAYS.  IN  AUGUST 1974  THE UNIT  WAS  TESTED
                      FOR TWO  DAYS  USING WESTERN  LOW-SULFUR  COAL.  THE  TEST SHOWED  ABOUT  50%
                      sos REMOVAL  EFFICIENCY!  BUT PRECIPITATOR PERFORMANCE WAS ADVERSELY
                      AFFECTED.  THE FGD PROJECT  HAS BEEN SHUT DOWN  INDEFINITELY  SINCE
                      AUGUST 1974,  AND  THERE  ARE  NO  PLANS FOR FUTURE OPERATION.
                                             179

-------
                 TABLE \Z
DESCRIPTION OF TERMINATED FGD SYSTEMS  01/78
UTILITY NAME

UNIT NAME

UNIT LOCATION

UNIT RATING

FUEL CHARACTERISTICS

FGD VENDOR

PROCESS

NEW OR RETROFIT

START UP DATE

FGD STATUS

EFFICIENCY,
 PARTICULATES
DETROIT EDISON

ST. CLAIR NO 6

BELLE RIVER MICHIGAN

 163 MW

COAL 0.3 PERCENT SULFUR

PEABODY ENGINEERING

LIMESTONE SCRUBBING

RETROFIT

 5/76

TERMINATED


99.7 PERCENT
  502
                      90 PERCENT
MATER MAKE UP
                      OPEN LOOP  1.07 GPM/MW
 SLUDGE  DISPOSAL
10-ACRE SETTLING POND
 UNIT  COST
                      SEE  APPENDIX A, FGD SYSTEM ECONOMICS
 OPERATIONAL
 EXPERIENCE
REFER TO THE BACKGROUND INFORMATION SECTION IN TABLE  12 OF THIS REPORT.
FOLLOWING THE COMPLETION OF A TWO MONTH INTERNAL S02  SCRUBBING DEMONSTRA-
TION PROGRAM THE SCRUBBER PLANT WAS BYPASSED.  MODIFICATIONS WERE
IMPLEMENTED TO OPERATE IN THE PARTICULATE MODE ONLY.  VENTURI SCRUBBERS
FOR PARTICULATE REMOVAL WERE PUT BACK IN OPERATION IN OCTOBER  1977. SPRAY
TOWERS ARE NOT COUPLED INTO THE SCRUBBING SYSTEM.  THE BOILER  IS NOW FIN-
ING LOW-SULFUR (0.3 PERCENT) WESTERN CDECKER) COAL.   COMPLIANCE WITH S02
REGULATIONS IS BEING ACHIEVED WITHOUT THE NECESSITY OF SCRUBBING.
                                              180

-------
                                       BACKGROUND  INFORMATION
                                                 ON
                                          ST. CLAIR  NO.  6

     THE  ST.  CLAIR  POWER PLANT OF THE DETROIT EDISON  COMPANY  IS  LOCATED  ON  THE  ST.  CLAIR  RIVER  IN
BELLE  RIVER,  MICHIGAN,  APPROXIMATELY 45 MILES NORTHEAST  OF  DOWNTOWN  DETROIT.   THIS  PLANT  CONTAINS  7
FOSSIL-FUEL-FIRED  GENERATING UNITS WHICH HAVE A  TOTAL NET  GENERATING CAPACITY  OF  1775-Mw.   UNIT  NO.
6 IS  A COAL-FIREO  TWO-STAGE SUPERHEATER UNIT, CONTAINING TWO  SEPERATE BOILER  BOXES  KNOWN  AS THE
SOUTH  BOILER  AND THE NORTH BOILER.  THE TOTAL NET  GENERATING  CAPACITY OF THE  NO.  6  UNIT  IS  325  MW.
THE SUPERHEATER WAS MANUFACTURED BY COMBUSTION ENGINEERING  AND  PLACED IN SERVICE  IN 1961.   BOTH  THE
NORTH BOILER  AND THE SOUTH BOILER ARE EQUIPPED WITH  EMISSION  CONTROL SYSTEMS.   THE  UNIT  CURRENTLY
OPERATES  AT  EXCESS  AIR RATES OF 115 TO 120 PERCENT.

     THE  ST.  CLAIR  NO. b BOILER FIRES EXCLUSIVELY  A  LOW  SULFUR  WESTERN SUBBITUMINOUS COAL  ORIGINAT-
ING FROM  DECKER COMPANY'S DIETZ MINE LOCATED  IN  SOUTHERN MONTANA.   THE AVERAGE  CHARACTERISTICS  OF
THIS COAL ARE:  HEAT CONTENT 9500 TO 9600 BTU/LB; SULFUR  CONTENT  OF  0.3 TO 0.4  PERCENT;  ASH  CUNTENT
OF 4.0 PERCENT! AND A TOTAL MOISTURE CONTENT  OF  22.0  TO  24.0  PERCENT.

     THE  EMISSION CONTROL SYSTEM INSTALLED ON THE  NORTH  BOILER  CONSISTS  OF  MECHANICAL COLLECTORS AND
AN ELECTROSTATIC PRECIPITATOR  (ESP) INSTALLED UPSTREAM OF  A WET  SCRUBBING SYSTEM.   THE  MECHANICAL
COLLECTORS AND  ESP ARE PROVIDED FOR PRIMARY PARTICULATE  CONTROL  THE  WET  SCRUBBING SYSTEM  PROVIDES
ADDITIONAL PARTICULATE REMOVAL AND PRIMARY DIOXIDE CONTROL.

     THE  FLUE GAS DESULFURIZATION  (FGD) CONSISTS OF  TWO  PEAdOOY-LURGI VENTURI  SCRUBBER  AND  SPRAY
TOWER ABSORBER  MODULES WITH A  TOTAL FLUE GAS  CAPACITY OF 493,500 ACFM AT 270  F.  THIS VOLUME IS
 EUUIVALENT TO APPROXIMATELY so PERCENT OF  THE TOTAL  FLUE GAS  FROM  THE NO. & UNIT.   THE  DESIGN FLOW
 RATE PER SCRUBBING TRAIN  IS 246,700 ACFM AT 270  F.  FLUE GAS  CAN BE  BYPASSED  AROUND THE  SCRUBBING
 SYSTEM.  6.6 MW OF ELECTRICAL  POWER ARE CONSUMED BY  THE  SCRUBBING  OPERATIONS.   THIS FGO  SYSTEM  IS  AN
 EXPERIMENTAL DEMONSTRATION UNIT DESIGNED AND  INSTALLED BY  PEABODY  ENGINEERED  SYSTEMS IN  COOPERATION
 WITH  THE DETROIT EDISON COMPANY.   EACH SCRUBBING TRAIN INCLUDES  A  CLEAR  WATER  TRAY  ANO
 RADIAL VANE MIST ELIMINATOR,  A COMMON RECYCLE TANK,  INDUCED DRAFT  FAN, OIL-FIRED  HOT-AIR-INJECT ION
 REHEAT SYSTEM AND A  10.6-ACRE  CLAY-LINED SETTLING  POND.   DESIGN  REMOVAL  EFFICIENCY  OF THIS  EMISSION
 CONTROL  SYSTEM  IS 99.7 PERCENT FOR  PARTICULATES  AND  90 PERCENT  FOR  SULFUR DIOXIDE BASED  UPON HI&H
 SULFUR EASTERN  COAL.  A DIAGRAM OF  ONE OF  THE TWO  PARALLEL SCRUBBING TRAINS 13  PRESENTED  IN
 APPENDIX B.
                                                  181

-------
DETROIT EDISON                         FGD SYSTEM  PERFORMANCE              ST.  CLAlR UNIT NO. 6

PERIOD                                               COMMENTS
MOV. 71       INSTALLATION OF THE FGD SYSTEM  WAS ESSENTIALLY COMPLETED  BY  THIS TIME.  A CAULIT
DEC. 74       INSTRUMENT PANEL WHICH WAS  INCORRECTLY  WIRED  HAS  BEEN  RETURNED TO THE MANUFACTURER
JAN. 75       FOR REPAIR.  TO DATE, THE UTILITY HAS  WATER TESTED  ALL THE  AUXILIARY EQUIPMENT.  THE
              I.D. FAN HAS BEEN TESTED AND AIR BALANCE  HAS  BEEN CHECKED.

FEB. 75
MAR. 75       A COLD FLUE GAS RUN WAS SUCCESSFULLY CONDUCTED MAK.  32-23.   DURING THIS PERIOD. THE
APR. 75       RUBBER-LINED PUMPS WERE REPAIRED AND THE  LIMESTONE  PREPARATION SYSTEM WAS CALIBRATED.

MAY  75
JUN. 75       THE FIRST HOT FLUE GAS RUN  WAS  CONDUCTED  ON JUNE  22,  1975.   THE  RUN LASTED FOR A
JUL. 75       PERIOD OF 22 HOURS.  DURING THIS RUN,  THE  SCRUBBER  WAS PURPOSELY TRIPPED OFF AT LOADS
              OF 40 AND 80 PERCENT.  THIS WAS PERFORMED  TO  OBSERVE  IF ANY  DETRIMENTAL EFFECTS TO
              THE STEAM GENERATION OPERATIONS RESULTED.  NONE WERE DETECTED.  THE SYSTEM WAS TAKEN
              OUT OF SERVICE FOLLOWING THIS GAS RUN  TO  CORRECT  THE FOLLOWING MAJOR OPERATION AREAS:
                  *GAS CIRCUIT: LURGI THROAT  POSITIONAL  FAILURE;  DETERIORATION OF THE DAMPEK SEALS;
                   SEVERE DUCT VIBRATIONS; S02 ANALYZERS INOPERATIVE.
                  •LIQUID CIRCUIT: FAILURE OF PH CONTROL SYSTEM;  TARGET FLOW METER TARGETS HAVE
                   BEEN BROKEN OFF; PUMP  SEAL WATER  LOW  FLOW ALARM  TRIPS.

AUG. 75       A SECOND HOT FLUE GAS RUN WAS INITIATED ON AUGUST 6  AND LASTED 27 HOURS.  THE RUN HAS
              TERMINATED BECAUSE OF A REHEA1ER THERMOCOUPLE FAILURE. A SUBSEQUENT INSPECTION OF
              THE SCRUBBING SYSTEM REVEALED NO APPARENT  ABNORMALITIES OR  MALFUNCTIONS.

SEP. 75
              A THIRD HOT FLUE GAS RUN OF 41  HOURS DURATION WAS COMPLETED  OCTOBER 9.  THE  MAIN
              OBJECTIVE OF THIS RUN WAS TO EVALUATE  VARIOUS COMPONENTS  OF  THE  FRESH WATER  SPRAY
              SYSTEM AND EFFECTS ON SYSTEM OPERATION.   THE  TEST RUN  WAS PREMATURELY TERMINATED BE-
              CAUSE OF A BOILER FEED PUMP MALFUNCTION,  RESULTING  IN  A REDUCED  BOILER LOAD  CAUSING
              SUBSEQUENT WEEPING OF THE WASH  TRAY.

NOV. 75

DEC. 75       A FOURTH FLUE GAS RUN OF 23 DAYS DURATION  WAS TERMINATED  DUE  TO  EXCESSIVE VIBRATION
              IN THE I.D. BOOSTER FAN.  ONE OTHER  SCRUBBER-RELATED OUTAGE  OCCURRED WHEN THE PACKING
              OF ONE OF THE SCRUBBER RECIRCULATION PUMPS NEEDED MAINTENANCE.  SOS REMOVAL  DURING
              THIS PERIOD WAS 9U PERCENT  AND  PAKTICULATE OUTLET LOADING WAS  0.1 L6/1UOO L8S OF FLUE
              GAS FOR 1-3 PERCENT SULFUR  CUAL.

JAN. 76

FEB. 76

MAR.  76

APR. 76       THE 30-DAY VENDOR QUALIFICATION RUN  AND FINAL ACCEPTANCE  TEST  WERE COMPLETED BY MAY
              29.  THE QUALIFICATION RUN  WAS  CONDUCTED  ON A "HANDS OFF" BASIS  USING PLANT  PERSONNEL
              EXCLUSIVELY.  THE SYSTEM WAS IN SERVICE 100 PERCENT  OF THE  TIME  THE BOILER WAS
              OPERATIONAL.  THE FINAL ACCEPTANCE IEST CONSISTED OF SIX  4-HR. TEST RUNS CONDUCTED IN
              THE SPACE OF ONE WEEK.  THE S02 REMOVAL EFFICIENCY  FOR HIGH  SULFUR COAL WAS  90.9
              PERCENT.  PARTICULATE REMOVAL ALSO EXCEEDED DESIGN  LEVELS.   NO MAJOR MECHANICAL OR
              CHEMICAL-RELATED PROBLEMS WERE  ENCOUNTERED.

JUN. 76

JUL. 76

AUG. 7fa       THE UTILITY IS NOW PREPARING TU CONDUCT A  2 MONTH MINIMUM INTERNAL SCRUBBER  DEMONSTRA-
              TION PROGRAM TO ACQUIRE OPERATING DATA  AND INFORMATION.   FOLLOWING THE COMPLETION OF
              THIS PROGRAM THE BOILERS WILL FIRE LOW  SULFUR DECKER COAL (0.3 TO 0.4 PERCENT) TO MEET
              so2 EMISSION REGULATIUNS.   THE  SCRUBBERS  WILL CONTINUE TO OPERATE IN THE PARTICULATE
              REMOVAL MODE

SEP. 7fa       THE INTERNAL S02 SCRUBBING  DEMONSTRATION  PROGRAM  COMMENCED  ON  OCTOBER 14.  THE SCRUB-
OCT. 76       BERS OPERATED CONTINUOUSLY  FOR  10 DAYS.   OPERATION  WAS INTERRUPTED BY A FORCED SCRUB-
              BER OUTAGE RESULTING FROM SCALE AND  SOLIDS CARRYOVER  FROM THE  WASH TRAY AND  MIST
              ELIMINATOR TO THE SCRUBBER  I.D. BOOSTER FAN ASSEMBLY,  CAUSING  VIBRATION AND  BALANCE
              PROBLEMS.  IT WAS DECIDED TO SANDBLAST  THE FAN TO REMOVE  SOLIDS  BUILDUP ON IHE FAN
              ASSEMBLY.  THE UTILITY PLANS TO MODIFY  THE COMPONENT'S WASH  SYSTEM FOR GREATER FLOW
              CAPABILITY AFTER COMPLETION OF  THE S02  SCRUBBING  PROGRAM.   DECO  ALSO PLANS TO CON-
              TINUE PARTICULATE SCRUBBING FOLLOWING  THE  TERMINATION  OF  THE S0e> PROGRAM BY  UNCOUPLING
              THE SPRAY TOWERS AND MAINTAINING THE PEABUDY-LURGI  VENTURI  SCRUBBERS IN THE  FLUE GAS
              STREAM.  SOME LIMESTONE MAY HAVE TO  BE  ADDED  TO THE PARTICULATE  SCRUBBING SOLUTION
              IN ORDER TO PREVENT LOW PH  SWINGS AND  MINIMIZE THE  POSSIBILITY UF ACID CORROSION
              DAMAGE TO THE INTERNAL COMPONENTS.
                                                  182

-------
DETROIT  EDISON                                                   ST. CLAIR UNIT NO. 6

PERIOD                                               COMMENTS
MOV.  76       FOLLOWING THE COMPLETION OF SAND BLASTING OPERATIONS  TO  SCRUBBER'S  I.D. BOOSTER FAN
             FOR REMOVAL OF SOLIOS 8U1LD (if, OPERATIONS RESUMED ON NOVEMBER 7 AND CONTINUED
              THROUGHOUT THE MONTH.  THE SYSTEM'S AVAILABILITY  INDEX FUR THE MONTH WAS 80 PERCENT
             THE MAJORITY UF THE OUTAGE TIME WAS CONSUMED PROCURING SAND BLASTING SERVICES.  THE
             OPERATION ITSELF REUUIREO ONLY tt HOURS.

DEC.  76        THE S02 DEMONSTRATION PROGRAM CONTINUED THROUGHOUT DECEMBER.  THE SYSTEM'S AVAILABIL-
              ITY INDEX FOR THE PERIOD WAS 51 PERCENT.  SCRUBBER OUTAGES RESULTED FROM MALFUNCTIONS
             OF THE LIMESTONt FEEDER, THE DENSE SLURRY TRAVERSE PUMP, THE DENSE  SLURRY TANK
              AGITATORS, AND PLUGGING OF THE PH SAMPLE LINE.

JAN,  77        THE 503 DEMONSTRATION PROGRAM WAS OFFICIALLY TERMINATED  ON DEC. 31, 1976.  THE SCRUB-
FEB.  77        BER PLANT WAS SHUT DOWN AT THIS POINT AND FLUE GAS WAS BY-PASSED AROUND THE SYSTEM.

MAR.  77        THE BOILER REMAINS IN SERVICE, FIRING LOW SULFUR  (0.3%)  WESTERN COAL.  CURRENT PLANS
              CALL FOR IHE SCRUBBER PLANT TO REMAIN 001 OF SERVICE  UNTIL MID-JUNE FOR DESIGN AND
              OPERATIONS MODIFICATIONS.  RESUMPTION OF SCRUBBER OPERATIONS WILL OCCUR IN TtiE PRI-
              MARY PARTICULATE-REMOVAL MODE.  THE PEABOOY-LURGI VENTURI SCRUBbERS AND SpRAY TOhER
              ABSORBERS WILL REMAIN IN THE GAS STREAM.  SOLUTION WILL  BE CIRCULATED THROUGH THE
              VENTURI'S, WASH TRAYS, AND MIST ELIMINATORS.  NO  SOLUTION WILL BE CIRCULATED THROUGH
              THE SPRAY ZONE OF THE ABSORBER TOWERS.  LIMESTONE REAGENT WILL BE ADDED TO THE
              SCRUBBING SOLUTION IN ORDER TO PREVENT LOW PH SWINGS  AND SUBSEQUENT MATERIALS DAMAGE
              TO THE SCRUBBER'S INTERNALS,  S02 REMOVAL SHOULD  RESIDE  IN THE 35 TO 50* RANGE IN
              THIS MODE OF OPERATION BECAUSE OF THE SOLUTION'S  ALKALINITY DUE TO  THE FLY ASH AND
              LIMESTONE.   ALSO DECO PLANS TO MAINTAIN A HIGHER  L/G  RATIO IN THE SCRUBBER MODULES.
              THIS MODE OF OPERATION IS PROJECTED TO CONTINUE FOR A ONE TO THREE-YEAR PtRIOO FOLLOW-
              ING THE MID-JONE RESTART.
                                                  1S3

-------
                 TABLE 12
DESCRIPTION OF TERMINATED FGD SYSTEMS   01/76
UTILITY NAME

UNIT NAME

UNIT LOCATION

UNIT RATING

FUEL CHARACTERISTICS

FGD VENDOR

PROCESS

NEW OR RETROFIT

START UP DATE

FED STATUS

EFFICIENCY,
 PARTICULATES
                      GULF POWER CO.

                      SCHOLi! NO. 1A

                      CHATTAHOOCHtE FLORIDA

                        20 MW

                      COAL   3.0 PERCENT  SULFUR

                      ADL/COMbUST ION EQUIP ASSOCIATE

                      OOUbLE ALKALI SCRUBBING

                      RETROFIT

                       2/7b

                      TERMINATED


                      99.7 PERCENT
 302
                      95 PERCENT
WATER MAKE  UP
                      CLOSED  LOOP
 SLUDGE  DISPOSAL
                       ON-SITE  LINED DISPOSAL  POND
 UNIT  COST
OPERATIONAL
 EXPERIENCE
                       REFER  TO  THE  BACKGROUND  INFORMATION  SECTION  IN  TABLE  12  OF  THIS REPORT.
                       THIS PROTOTYPE  SCRUBBING  SYSTEM  WAS  INITIALLY  PLACED  IN  SERVICE FEBRUARY
                       1975 AND  WAS  OPERATIONAL  A  TOTAL  OF  4744  HOURS  IHRUUGHOUT  THE  YEAH.   THE
                       SYSTEM  REMAINED  IN  SERVICE  DURING  THE  FOLLOWING  b  MONTHS IN 1976.
                       SUCCESSFUL  COMPLETION  OF  THIS  PROGRAM  OCCURRED  ON  JULY  a,  is/b.  PRESENT
                       PLANS  CALL  FOR  A  FULL  SCALE  EPA-SPONSORED DEMONSTRATION  PROGRAM WITH
                       THE  INSTALLATION  SITE  BEING  LOUISVILLE  GAS &  ELECTRIC'S  CANt HUN STATION,
                       UNIT NO.  6.
                                              184

-------
                                       BACKGROUND  INFORMATION
                                                 ON
                              SCHOLZ CEA/ADL  DUAL  ALKALI  PHOTOTYPE

     THE  SCHOLZ  STEAM POWER PLANT OF GULF POWER COMPANY  IS LOCATED  IN CHATTAHUOCHEE,  FLOKIDA.   UNIT
NO.  1  IS  A  COLA-FIRED STEAM BOILEK DESIGNED AND INSTALLED  BY BABCOCK  AND wILCUX  IN 1953.   THIS UNIT
IS NORMALLY  RATED  AT 
-------
GULF POWER CO.
                                      SCHOLZ  1A  -  DOUBLE  ALKALI
                                                                                SCHOLZ UNIT NO. U
  PERIOD
          TOTAL
          HOURS
  UNIT OPERATING HOURS

BOILERS  FGD SYSTEM
                                   FGD SYSTEM
                                  OPERABIL1TY
                                               PERFORMANCE  CX)
                                                UTILIZATION
FEB.
MAR.
APR.
MAY
JUN.
JUL.
AUG.
SEP.
OCT.
NOV.
DEC,
           672
           744
           720
           744
           720
           744
 459
 507
 604
 598
 720
 663
                        454
                        485
                        336
                        375
                        720
                        221
UNIT WAS PLACED IN OPERATION FtB. e,
FOR 2 MONTHS MODIFICATIONS, REPAIRS,
                                      99            68
                                      9fo           665
                                      56            47
                                      63            50
                                     100           100
                                      32            30
                                     1975 AND OPERATED UNTIL JULY  18 WHEN  IT  WAS  SHUT  DOWN
                    	 	 AND REPLACEMENT OF PARTS.  THE SYSTEM  WAS  UNAVAILABLE
TO THE BOILER FOR A 491-HR PERIOD BECAUSE OF ADJUSTMENTS AND MODIFICATIONS  REQUIRED  FOR  THE
FORMAL EPA TEST PROGRAM IN MID-MAY.
     75    744      744          000
     75    720      577        254           44            35
     75    744      559        559          100            75
       THE SYSTEM WAS SHUT DOWN FROM MID-JULY TO MID-SEPTEMBER FOR MECHANICAL OVERHAUL INVOLVING
       REPLACEMENT PARTS FOR VALVES THAT HAD FAILED.  THE SYSTEM WAS PUT BACK IN OPERATION ON SEP
       16, 1975.  FROM MIO-SEP. TO MID-OCT.  THE AIR PREHEATER WAS REPAIRED AND BOILER OPERATION
       ADJUSTED TO REDUCE OXYGEN LEVELS IN THE FLUE GAS TO THE 5 TO 6 PERCENT RANGE.  THE SYSTEM
       OPERATED APPROXIMATELY 800 HRS. DURING THI3PERIOD.

     75    720      620        560           90            78
     75    744      732        732          100            98
       THE SYSTEM RAN CONTINUOUSLY FOR THE REMAINDER OF THE TEST PERIOD THROUGH JANUARY ^, 1976.
       S02 LEVELS DURING THIS PERIOD RANGED FROM 800 TO 1700 PPM.  THE SYSTEM OPERATED IN THE
       CONCENTRATED MODE THROUGHOUT THE REMAINDER OF THE TEST PERIOD.  IN THE PERIOD FROM MID-SEP.
       TO JAN. 2, 1976, THE SYSTEM OPERATED ABOUT 2100 HRS., WITH AN UPERA8ILITY FACTOR OF 97
       PERCENT.

     76    744
     76    696
       THE FGO SYSTEM AND BOILER UNDERWENT A SCHEDULED OVERHAUL DURING THE REPORT PERIOD.  SYSTEM
       RESTART IS SCHEDULED FOR MID-MARCH 1976, TO CONTINUE UNTIL JUNE.  DURING THIS OPERATING
       PERIOD HIGH-SULFUR COAL [3.5-4.ox) WILL BE BURNED TO ALLOW EVALUATION OF SYSTEM PERFORMANCE
       ON HIGH SULFUR COAL.

     76    744      742        445           60            60
       THE SYSTEM WAS PUT BACK IN SERVICE ON MAR. 12, 1976.  THE TOTAL NUMBER OF OPERATING HRS. FOR
       THE MONTH OF MAR. WAS 445 HRS.  THIS TRANSLATES INTO A 94X OPERABILITY FACTOR SINCE THE
       MAR. 12 RESTART.

APR. 76    720      642        616           96            86
MAY. 76    744      735        651           89            68
       SOME MINOR MECHANICAL PROBLEMS IN THE FORM OF AGITATOR SHAFT AND CONTROL VALUE FAILURES WERE
       ENCOUNTERED DURING THE REPORT PERIOD.  SINCE THE SYSTEM RESTART ON MARCH. 12, HIGH-SULFUR
       COAL HAS BEEN BURNED IN THE BOILER 13.5 TO 4.5X SULFUR), RESULTING IN THE S02 INLET
       CONCENTRATION LEVELS IN THE 2000 TO 2500 PPM RANGE.

JUN. 76    720      656        641           93            89
       DURING THE LAST PHASE OF OPERATION, THE SYSTEM WAS TREATING FLUE GAS OF VARYING PARTICULATE
       LOADS.  THE UPSTREAM ESP WAS SELECTIVELY DE-ENERUIZED, BOTH PARTIALLY AND TOTALLY, NO MAJOR
       UPSETS IN THE PROCESS CHEMISTRY OCCURRED.  BOILER LOAD VARIATION RANGED FROM 30 TO 100X.  THE
       PROTOTYPE PROGRAM AT THE PLANT WAS SUCCESSFULLY CONDUCTED ON JULY 2.  ADL IS CURRENTLY
       COMPLETING DATA ACQUISTION AND ANALYSIS.

JUL. 76    744       54         54          100
       THE PROTOTYPE TEST PROGRAM WAS SUCCESSFULLY CONCLUDED ON JULY 3, 1976.
       NOTE:   THE BOILER HRS., SYSTEM OP HRS., AND THE CORRESPONDING PERFORMANCE VALUE CALCULATED
              INCLUDES SYSTEM OP UP TO THE SCHEDULED SHUTDOWN, ON JULY 3, 6 O'CLOCK A.M., 1976.
JAN.
FEB.
MAR.
                                                 186

-------
                 TABLE 13
DESCRIPTION OF TERMINATED FGO SYSTEMS   01/78
UTILITY NAME

UNIT NAME

UNIT LOCATION

UNIT RATING

FUEL CHARACTERISTICS

F6D VENDOR

PROCESS

NEW OR RETROFIT

START UP DATE

FGO STATUS

EFFICIENCY,
  PARTICULATES
GULF POWER CO.

SCHULZ NO. 2A

CHATTAHOOCHfcE FLORIDA

  20 MM

COAL   3.0 PERCENT SULFUR

FOSTER WHEELER

ACTIVATED CARBON

RETROFIT

 2/76

TERMINATED


99.7 PERCENT
  S02
                      74.5  PERCENT  [DESIGN)
 MATER MAKE UP
                      N/A  DRY  ADSORPTION  SYSTEM
 SLUDGE DISPOSAL
                      MOLTEN  ELEMENTAL  SULFUR
 UNIT COST
                      SEE  APPENDIX  A,  FGO  SYSTEM ECONOMICS
 OPERATIONAL
  EXPERIENCE
REFER TO THE BACKGROUND  INFORMATION SECTION  IN TABLE RED IN AUGUST 1975,
REPORT.  THIS  IS A PROTOTYPE DRY ADSORPTION  REGENERABLE SYSTEM
DESIGNED BY FOSTER WHEELER AND BERGBAU FORSCHUNG.  OPERATION OF
THE PROTOTYPE  UNIT DURING THE SCHOLZ DEMONSTRATION PROGRAM PROCEEDED
ON AN INTERMITTtNT BASIS.  OPERATIONAL SEGMENTS OCCUKEO IN AUGUST 1975,
OCTOBER 1975,  AND MARCH, APRIL AND MAY 1976.  SYSTEM OPERATIONS WERE
PREMATURELY TERMINATED AT THIS POINT AND THE PROTOTYPE UNIT WAS SHUT
DOWN.  THE SYSTEM IS CURRENTLY INACTIVE.
                                              187

-------
                                       BACKGROUND INFORMATION
                                                 UN
                               SCHOLZ FWBF DRY ADSORPTION PROTOTYPE

     IN JANUARY 1973, THE SOUTHERN SERVICES COMPANY OF GULF POWER AWARDED  A CONTRACT  TO  THE FOSTER
WHEELER CORPORATION TO BUILD A 20-MW PROTOTYPE DRY ADSORPTION SYSTEM FOR FLUE  GAS  DESULFUKIZATION.
CONSTRUCTION ON THE FOSTER WHEELER PROCESS STARTEDFEBRUARY 15,  1974, AT THE SCHOLZ  STEAM POWER PLANT
IN CHATTACHOOCHEE, FLA.  CONSTRUCTION WAS COMPLETED AND A TESTING PROGRAM  WAS  INITIATED  IN  MAY 1975.

     THE SYSTEM AT THE SCHOLZ PLANT CONSISTS OF A 20-MW ADSORBER SECTION AND A 47.5-Mw REGENERATION
AND REDUCTION SECTION.  THE 20 MW ADSORBER IS DESIGNED TO ACCEPT HALF OF THE MAXIMUM  FLUE GAS  FLOW
FROM UNIT NO. 2.  THE COAL-FIRED BOILER IS RATED AT 40 MW (NOMINAL)* IT FIRES  COAL  WITH  AN  AVERAGE
HEATING VALUE OF 12,400 BTU/LB.  MAXIMUM ASH AND SULFUR CONTENTS ARE 14 AND 5  PERCENT, RESPECTIVELY.

     THE PURPOSE OF THE ADSORPTION SECTION OF THE FWBF DRY REMOVAL SYSTEM  IS TO REMOVE SULFUR
DIOXIDE, NITROGEN OXIDES, AND PARTICULATE FROM THE FLUE GAS WITH ACTIVATED CHAR, CONVERTING  THE
CAPTURED POLLUTANTS TO SULFURIC ACID.  THE REGENERATION SECTION PROVIDES CONTINUOUS OlM-SITE  REGENER-
ATION OF THE CHAR, WHICH HAS BEEN LOADED WITH SULFUR DIOXIDE IN THE FORM OF SULFURIC  ACID.   THE CHAK
IS REGENERATED AND A LOW-VOLUME, SULFUR DIOXIDE-RICH OFF-GAS STREAM IS FED FORWARD  TO THE RESQX
REACTOR, WHICH REDUCES THE SULFUR DIOXIDE STREAM TO GASEOUS ELEMENTAL SULFUR THAT  IS  COLLECTED AND
STORED  IN AN INSULATED TANK.

     THE DEMONSTRATION UNIT HAS TWO ROWS OF MODULES, EASH ROW CONSISTING OF SIX MODULES,  THE
ADSORPTION SECTION IS A TWO-STAGE DESIGN CONSISTING OF VERTICAL COLUMNS OF PARALLEL LOUVER  BEDS
WHICH SUPPORT AND CONTAIN THE ACTIVATED CHARCOAL.  SULFUR DIOXIDE, OXYGEN, WATER VAPOR,  AND  NITROGEN
OXIDES  ARE ADSORBED BY THE CHAR PELLETS FROM THE CROSS-FLOWING FLUE GAS AT 250 TO  300 F.  THE  SULFUR
DIOXIDE THEN REACTS WITH OXYGEN AND WATER TO FORM SULFURIC ACID WHICH IS FIRMLY RETAINED  IN  THE INT-
ERIOR PORE SYSTEM OF THE CHAR PELLETS.  THE CHAR IS THEN REGENERATED IN THE REGENERATOR  VESSEL BY
HEATING TO 1200 F, DRIVING OFF THE ENTRAINED GASES, AND REDUCING SULFURIC  ACID TO SULFUR DIOXIDE.
THE SULFUR OIOXIDE-RICH GAS IS THEN PASSED THROUGH A VESSEL CONTAINING CRUSHED COAL,  RESULTING IN
REDUCTION TO GASEOUS ELEMENTAL SULFUR AND CARBON DIOXIDE.  THIS LATTER PROCESS IS CARRIED OUT  AT
1200 TO 1500 F.  A SCHEMATIC OF THE PROCESS COMPONENTS FOR THE FW-8F DRY ADSORPTION IS PRESENTED IN
APPENDIX B.

     THE INITIAL SHAKEDOWN ON FLUE GAS BEGAN AUG. 11, 1975, AND PROCEEDED  CONTINUOUSLY FOR  10  DAYS.
THE REGENERATION SECTION WAS OPERATIONAL ABOUT 60 PERCENT OF THE TIME.  HOWEVER, THE  REDUCTION SEC-
TION HAS NOT YET BEEN INTEGRATED INTO SYSTEM OPERATION.  SULFUR DIOXIDE REMOVAL WAS WELL ABOVE EX-
PECTATIONS AND PRESSURE DROP ACROSS THE ADSORBER WAS nELL BELOW DESIGN LEVELS.  THE SYSTEM WAS SHUT
DOWN FOR CORRECTION OF SEVERAL OPERATING PROBLEMS, EQUIPMENT MODIFICATIONS, AND EVALUATION OF  THE
INITIAL OPERATING DATA.  OPERATION WAS RESUMED IN OCTOBER 1975, WHEN TWO CONSECUTIVE RUNS WERE COND-
UCTED WITH THE REDUCTION PORTION OF THE SYSTEM PROCESSING FRONT-END OFF-GAS AT FULL OPERATING  TEMP-
ERATURES.  A PROGRAM OF MODIFICATION WAS COMPLETED ON THIS SYSTEM IN EARLY JANUARY  1976.  REINTROD-
UCTION  OF FLUE GAS INTO THE INTEGRATED SYSTEM COMMENCED IN FEBRUARY 1976.  OPERATIONS THROUGH  A
FINAL 4-MONTH TEST PROGRAM WERE PREMATURELY TERMINATED ON MAY 2, 1976.
                                                 188

-------
6ULF POWER  CO.                 FWBF SYSTEM OPERATING HISTORY      SCHOLZ UNIT NO. 2A

PERIOD                                          COMMENTS
MAY  75     COMPLETION OF CONSTRUCTION WAS FOLLOWED 8Y  A  3-MONTH COMMISSIONING PERIOD DURING WHICH
JUN. 75     VARIOUS PIECES OF EQUIPMENT WERE OPERATED  INDIVIDUALLY  AND  THEN  IN COMBINATIONS TO
JUU. 75     SIMULATE SUBSYSTEM OPERATION.  SUBSYSTEM OPERATIONS WERE  INTEGRATED  INTO SECTION OPERA-
AUC. 75     TIONS AND FLUE GAS WAS PASSED THROUGH THE  ABSORBER AND  REGENERATOR FOR A 10-DAY PERIOD
           BEGINNING AUGUST 11.  RESOX CONSTRUCTION WAS  INCOMPLETE AT  THIS  TIME.

OCT.  75     TWO CONSECUTIVE RUNS WERE CONDUCTED ON THE  RESOX  PORTION  OF THE  SYSTEM ON FRONT-END
           PROCESS OFF-6AS AT FULL OPERATING TEMPERATURES.   THIS OPERATIONAL PERIOD LASTED 5 DAYS.

NOV.  75     A PROGRAM OF MODIFICATIONS ON THE SYSTEM BEGAN  IN LATE  AUGUST  1975 AND CONTINUED THROUGH
DEC.  75     JAN. 1976, WITH THE EXCEPTION OF THE 5-DAY  RESOX  OPERATION  IN  OCTOBER.
JAN.  76     MODIFICATIONS WERE COMPLETED AND PRE-3TARTUP  TESTING WAS  CONDUCTED IN LATE JANUARY AND
           EARLY FEBRUARY.  A 3-OAY CONTINUOUS RUN WAS SUCCESSFULLY  COMPLETED.

FEB.  76     ALL MATERIALS-HANDLING LOOPS AND RESOX LOOPS  WERE OPERATED  AT  FULL OPERATING TEMPERATURES
           AND PRESSURES.  REENTRODUCTION OF FLUE GAS  INTO  THE SYSTEM  COMMENCED, AND A 1-MONTH
           FORMAL TEST PROGRAM CONDUCTED BY SOUTHERN  SERVICES AND  FOSTER  WHEELER IS NOW IN PROGRESS.

MAR. 76    THREE OPERATIONAL PERIODS HERE LOGGED BY THE  PROTOTYPE  SYSTEM  DURING THE REPORT MONTHS.
APR. 76    DURING THESE RUNS THE  ADSORPTION AND REGENERATION SECTIONS  PERFORMED ADEQUATELY.  THE
           RESOX SECTION OPERATED INTERMITTENTLY BECAUSE OF  PLUGGING PROBLEMS IN THE SULFUR CONDEN-
           SER.  ALSO, THE FRONT  END OF THE SYSTEM WAS TAKEN DOWN  AT ONE  POINT  DUE TO FREQUENT HIGH
           TEMPERATURE EXCURSIONS.  THIS PROBLEM WAS  CORRECTED BY  MODIFYING SYSTEM OPERATING PRO-
           CEDURES.  CURRENTLY,  WORK IS PROCEEDING ON THE  SOLUTION OF  THE SULFUR CONDENSER PROBLEM.

 MAY  76    THE FW-BF UNIT  COMPLETED AN  OPERATIONAL PERIOD  IN EARLY MAY WHICH HAD COMMENCED ON APRIL
           26.  THE  SYSTEM WAS TAKEN DOWN  AT THIS POINT  FOR  THE FOLLOWING REASONS:
           *   DEPLETION OF CHAR  SUPPLY.
           *   HIGH  CHAR CONSUMPTION RATES  DUE  TO MECHANICAL ATTRITION.
           *   CORRECT/MODIFY  THE CHAR/SAND SCREEN SEPARATOR.
           AT  THIS  POINT THE DECISION WAS  MADE  TO PREMATURELY TERMINATE THE Frt-BF DEMONSTRATION
           PROGRAM  RATHER  THAN SHUT DOWN,  DEBUG,  AND  RESTART THE  SYSTEM AGAIN.  THE SYSTEM SUPPLIER
            IS  PURSUING  ADDITIONAL FUNDING  FOR  THE CONTINUATION OF  THE  PROTOTYPE DEMONSTRATION
           PROGRAM.
                                                  189

-------
                 TABLE 12
DESCRIPTION OF TERMINATED F6D SYSTEMS  01/78
UTILITY NAME

UNIT NAME

UNIT LOCATION

UNIT RATING

FUEL CHARACTERISTICS

F6D VENDOR

PROCESS

NtW OR RETROFIT

START UP DATE

F6D STATUS

EFFICIENCY,
 PARTICULATES
 GULF  POWER CO.

 SCHOLZ  NOS. IB  & 2B

 CMATTAHOOCHEE FLORIDA

   23  MW

 COAL  5.0 PERCENT SULFUR (MAX)

 CHIYODA INTERNATIONAL

 THOROUGHBRED 101

 RETROFIT

  3/75

 TERMINATED


 99.7  PERCENT
 S02
                      90 PERCENT
WATER MAKE UP
                      OPEN LOOP
 SLUDGE  DISPOSAL
                      DRY GYPSUM POND
 UNIT  COST
SEE APPENDIX A,  FGD SYSTEM ECONOMICS
 OPERATIONAL
  EXPERIENCE
 REFER TO THE BACKGROUND INFORMATION
 AND GULF POWER ANNOUNCED ON MARCH 22
 PROGRAM.  DURING JANUARY,  FEBRUARY,
 20 MINUTES OF FORCED SCRUBBER OUTAGE
 PERCENT UNTIL PROGRAM TERMINATION.
 PERCENT FROM OCT. 17 THROUGH PROGRAM
 ABANDONED THE 101 PROCESS  DESIGN IN
 INCORPORATES LIMESTONE SCRUBBING IN
IN TABLE 12 OF THIS REPORT.  CHIYODA
 THE COMPLETION OF THIS DEMONSTRATION
AND MARCH OPERATIONS, THERE WERE ONLY
.  UTILIZATION WAS ESSENTIALLY 100
PROCESS UTILIZATION WAS GREATER THAN
 COMPLETION.  CHIYODA HAS SINCE
FAVOR OF THE 121 PROCESS DESIGN WHICH
A JET BUBBLER REACTOR.
                                              190

-------
                                       BACKGROUND  INFORMATION
                                                 ON
                                   SCHOLZ UMTS  1  AND  i.  •  CHIYOOA

     THE  SCHOLZ  POWER PLANT IS LOCATED IN CHATTAHOOCHEE, FLORIDA,  ABOUT  SO  MILES WEST  UF
TALLAHASSEE.   THE FGD SYSTEM WAS DESIGNED BY  CHIYOOA  INTERNATIONAL CORP.,  FOR TESTING  AMD  PROCESS
DEMONSTRATION ON A COAL-FIRED APPLICATION.   THE  PROCESS  IS USED  IN JAPAN EXCLUSIVELY  ON OIL-FIRED
AND GAS-FIRED BOILERS, AND TAIL GAS FROM CLAUS UNITS.

     THE  SYSTEM  AT SCHOLZ CAN HANOLE ONE-HALF THE  LOAD 153,000  SCFM)  FROM  EITHER OF THE <40-M«
NOMINALLY RATED  BOILERS, WHICH WERE DESIGNED  AND INSTALLED BY  BABCOCK AND  WILCOX IN 1953.   DESIGN
ABSORBER  INLET SULFUR OIOXIOE CONCENTRATION  IS cjaSO  PPM.   VARIOUS  TESTS  COALS WITH SULFUR  CONTENTS
RANGING UP TO 5  PERCENT ARE SCHEDULED FOR BURNING.

     THE  PARTICULATE LOADS FROM NEWLY INSTALLED  ELECTROSTATIC  PRECIPITATORS ON THE TWO UNITS RANGE
FROM 0.02 TO 0.1 GR/SCF.  FLUE GAS FROM  THE  PRECIPITATORS  IS QUENCHED WITH  COOLING WATER  TO REMOVE
ADDITIONAL FLY ASH AND TO COOL THE GAS BEFORE II ENTERS  THE SULFUR DIOXIDE  ABSORBER.

     SULFUR DIOXIDE  IS ABSORBED IN WATER AND  CATALYTICALLY OXIDIZED WITH AIR TO FURM  SULFURIC  ACIU.
THE DILUTE ACID  IS RECIRCULATEO THROUGH  THE  ABSORBER.   A PORTION OF THE  ACID IS NEUTRALIZED WITH
LIMESTONE TO PRODUCE GYPSUM AS A BY-PRODUCT.

     BREAK-IN TESTING COMMENCED IN FEBRUARY  1975.   THE FIRST FEW MONTHS  OF  THE SHAKEDOWN  PERIOD  WERt
CHARACTERIZED BY MANY MINOR PROBLEMS, RESULTING  IN A  LOW OPERABILITY  INDEX  VALUE (30X  FUR  FtB-MAY).
MANY OF THESE PROBLEMS WERE RESOLVED BY  JUNE, (MANIFESTED  BY A  HIGHER OPERABILITY INDEX 18UX)  VALUE
FOR THE JUNE-JULY PERIOD).  A 6-WEEK SCRUBBER OUTAGE  PERIOD COMMENCED IN AUGUST FROM  UNBALANCING  UF
THE GYPSUM CENTRIFUGES.   AFTER REPAIR OF  THE CENTRIFUGES AND INSTALLATION  ON SEPTEMBER 15, THE UPtR-
ABILITY  INDEX THROUGH DECEMBER  1975, AVERAGED AbOVE  97 PERCENT.

     CHIYOOA, GULF POWER,  AND SOUTHERN  COMPANY SERVICES  SUCCESSFULLY  CONCLUDED CT-101  OPERATIONS  ON
MARCH  ZZ, 1977,   AFTER MORE  THAN TWO  YEARS  OF INTENSIVE TESTING,  EVALUATION, AND DEMONSTRAI ION.
 INFORMATION  AND  DATA CONCERNING THE  OPERATION OF THE  CT-101 PROTOTYPE UNIT  ARE PRESENTED  IN THE
PERFORMANCE  TABLE THAT  FOLLOWS.  A PROCESS  FLOW  DIAGRAM  IS PROVIDED IN APPENDIX B.
                                                  191

-------
GULF POWER CO.
                                    SCHOLZ  IB  AND  2B  -  CHIYODA
                                                                      SCHOLZ  UNIT NOS. IB AND 28
MONTH

FEB. 75
TOTAL
HOURS

 672
   UNIT OPERATING HOURS


BOILER        FGD SYSTEM
                                                          FGO  SYSTEM  PERFORMANCE  (X)
                                                          OPERABILITY         UTILIZATION
APR. 75
              720
                           720
                                           200
                                                              26
MAY  75       744          744              100                13                  13
       THIS IS A PILOT PLANT SIZE DEMONSTRATION  UNIT.  PRELIMINARY  ENGINEERING  AND DESIGN WORK BEGAN
       IN 1973.  INITIAL SHAKEDOWN AND DEBUGGING  OPERATIONS  COMMENCED  ON  FEBRUARY  11,  1975.  PROB-
       LEMS ENCOUNTERED INCLUDED CRACKS  IN  THE FRP LINING  AT  THE  OXIDIZING  TOWER.   STARTUP OCCURRED
       IN MARCH 1975.  AFTER INITIAL OPERATION FOR BREAK-IN  TESTS,  THE UNIT  WAS SHUT DOWN FOR IN-
       TERNAL INSPECTION.  RELIABILITY TESTS  THtN FOLLOWED IN  JULY  1975.  CHEMICAL PERFORMANCE WAS
       SATISFACTORY.  EMISSION TESTS HAVE NOT BEEN PERFORMED.  SOME PUMP  AND  INSTRUMENT FAILURES
       HAVE OCCURRED.
JUN. 75
JUL. 75
              720
              744
                          685
                           744
                                           685
                                           624
                                                            100
                                                              84
                                                                                95
                                                                                 84
       A  100 PERCENT OPERABILITY FACTOR WAS REGISTERED FOR  THE MONTH  Of  JUNE.   DURING  THE  MONTH  OF
       JULY ONE CENTRIFUGE BECAME UNBALANCED, REQUIRING  THE  SPARE  TO  BE  PLACED  IN  SERVICE.
 AUG.  75

 SEP.  75
              744
              720
                           720
                                            337
                                                                                 46
       DURING THE MONTH OF AUGUST BOTH CENTRIFUGES BECAME UNBALANCED  REQUIRING  A  FORCED  OUTAGE  WHICH
       EXTENDED  TO MID-SEPTEMBER.  UNIT OPERATED  AT  A 95 PERCENT  S02  REMOVAL  EFFICIENCY  DURING  THIS
       PERIOD.   GULF  POWER IS  ATTEMPTING  TO UPGRADE  THIS VALUE  TO  A HIGHER  EFFICIENCY  LEVEL.
 OCT.  75
              744
                            744
                                           744
                                                             100
        WASTE WATER DISCHARGE FROM THIS UNIT STILL A PROBLEM  AREA.
 NOV.  75
               720
                            720
                                          720
                                                             100
                                                                                 100
        OUTAGE  TIME WAS LESS  THAN ONE  HOUR DURING NOVEMBER OPERATION DUE  TO  A  BROKEN  FLUE  GAS  BLOWER
        INLET VANE AND REPAIR OF A PINHOLE IN  THE pRtscfiuBBER FRP LINING.
 DEC.  75
               744
                            744
                                          726
                                                             98
                                                                                  98
        SCRUBBER OUTAGES DURING DECEMBER RESULTED FROM CONTINUING REPAIRS  TO  A  PINHOLE  IN  THE
        PRESCRUBBER FRP LINING.
 JAN.  76
               744
                            680
                                           450
                                                              66
                                                                                  60
 FEB.  76        696           690              77                 11                   11
       OUTAGE  TIME  IN  JANUARY-FEBRUARY WAS  PRIMARILY FOR REPAIR  AND  MODIFICATION  OF  THE  SUCTION  AND
       DISCHARGE PIPING  ON  THE  ABSORBENT CIRCULATION PUMPS.   THESE FRP  LINES  BROKE  IN  JANUARY  AT
       SOME  WEAK FIELD JOINTS.   S02  REMOVAL EFFICIENCY HAS BEEN  AS HIGH  AS  95X.
 MAR.  76
               744
                            744
                                          741
                                                             100
                                                                                 100
 APR.  76       720            720             101                14                   14
       PLANT  WAS  STOPPED  APRIL 5 FOR  A SCHEDULED  SHUTDOWN  TO  ALLOW  INSTALLATION  AND  MODIFICATIONS
       FOR  REDUCING  THE QUANTITY OF LIQUID WASTE  FROM  THE  SYSTEM.   START-UP  AND  TESTING  OF  THIS
       MODIFICATION  WAS PLANNED FOR THE FIRST WEEK  IN  MAY.
       SITATED  A  DELAY IN SYSTEM RESTART FOR AN ADDITIONAL
                                                            A FIRE AT THE PLANT,
                                                           3 TO 4 WEEKS.
                                                                    HOWEVER, NECES-
 MAY  76
 JUN.  76
        THE  SYSTEM WAS SHUTDOWN APRIL 24 BECAUSE OF EXTENSIVE  FIRE  DAMAGE  IN  THE  OXIDIZING  TOWER.
        THE  FIRE, CAUSED BY  A WELDING ACCIDENT, DAMAGED FRP  AND POLYPROPYLENE  COMPONENTS  IN THE
        OXIDIZING TOWER.  REPAIRS CONTINUED  AS  THE SYSTEM  REMAINED  OUT  OF  SERVICE DURING  THE REPORT
        PERIOD.  SYSTEM RESTART IS SCHEDULED FOR THE END OF  JULY.

 JUL.  76

 AUG.  76       744           744              492                66                  66
        THE  PROTOTYPE UNIT REMAINED OUT OF SERVICE MAY, JUNE AND  JULY  TO REPAIR  THE  FIRE-DAMAGEO
        AREAS.  THE SYSTEM WAS PUT BACK IN OPERATION IN AUGUST.   THE SYSTEM WAS  AGAIN BROUGHT DOWN
        DURING THE MONTH TO  COMPLETE ADDITIONAL REPAIRS WHICH  WENT  UNDETECTED  DURING THE  PREVIOUS
        OUTAGE.  241.67 HOURS OF THE 251.75  HOURS OF AUGUST  OUTAGE  TIME WAS CONSUMED FOR  THESE
        ADDITIONAL REPAIRS.  THE WATER SAVINGS  PROGRAM IS  NOW  BEING CONDUCTED  ON  THIS SYSTEM.
        BASICALLY, THIS TEST PROGRAM CALLS FOR  A REDUCTION IN  WASTEWATER SLOWDOWN AND FRESH WATER
        MAKEUP REQUIREMENTS  BY RECYCLING THE MOTHER LIQUOR BLEED  BACK  TO THE  PROCESS FOR  ADDITIONAL
        SERVICE.
                                                  192

-------
GULF  POWER  CO.
                               SCHOLZ  18  AND  2B  -  CHIYUDA

             UNIT OPERATING HOURS
                                                                       SCHOLZ  UNIT  NOS.  IB  AND  2B
MONTH

SEP.


OCT.
        TOTAL
        HOURS
           BOILER   FGD SYSTEM
                     FGD SYSTEM PERFORMANCE CX)
         AVAILABILITY   OPERABILITY   RELIABILITY   UTILIZATION
76  720      720        496            99              69            99
  TOTAL FORCED OUTAGE TIME DURING  THE  MONTH  AMOUNTED TO 5.1  HOURS.
                                                         69
76  704      744         357            70              48            62            48
  TOTAL DOWN TIME DURING  THE  MONTH  AMOUNTED  TO  386.9 HOURS.   OF  THIS TOTAL  1.1  HOUR  WAS  AT-
  TRIBUTED TO A FORCED SCRUBBER  OUTAGE,  2ie  HOURS WAS REQUIRED TO REPAIR EXPECTED DAMAGES
  INCURRED IN THE PRESCRUBBER RESULTING  FROM OPERATIONS IN THE WATER SAVINGS  PROGRAM.  SPECI-
  FICALLY, THE LINING WAS  SUFFERING FROM  EXTENSIVE CORROSION DAMAGE BECAUSE  OF  HIGH  ACID
  CONCENTRATIONS WHICH DEVELOPED IN THE  PRtSCRUBBER SCRUBBER SOLUTION.   THIS  OUTAGE  WAS
  SCHEDULED FOR INSPECTION, REPAIR,  AND  PROVIDE DESIGN DATA  FOR  FUTURE  UNITS.   302 REMOVAL
  EFFICIENCY STILL RESIDES IN THE  85-95  PERCENT RANGE.
 NOV. 76  720
                  720
                              717
                                            99
                                                          99
                                                                        99
                                                                                      99
 DEC. 76  744      744         741            99             99             99             99
       A TOTAL OF THREE FORCED  SCRUBBtR  OUTAGES  OCCURRED RESULTING  IN OUTAGE  TIME  TOTALLING  6.5  HRS.
       PROBLEMS INCLUDED  A MALFUNCTION  OF  A LEVtL  INDICATOR,  A  BROKEN GUIDE  VANE,  AND AN  OPERATOR
       ERROR RESULTING  IN A  LEAK  OF  SLURRY  INTO  THE  WATER HEADER.   ON NOV.  1,  SOUTHERN SERVICES
       FINISHED ITS SCHOLZ EVALUATION OF  THE CT-101.   A  PERFORMANCE REPORT  IS  DUE  SPRING  1977.
       GULF POWER WILL  CONTINUE OPERATION  OF THE CHIYOOA UNIT  FUR  AN UNSPECIFIED PERIOD  IN  1977.
 JAN.  77  744

 FEB.  77  672
              744

              672
744

672
100

100
100

100
100

100
100

100
 MAR.  77   744       744         514           100                         100
       CICr GPC,  &  SCS  SUCCESSFULLY  CONCLUDED THE CT-101  TESTING AND DEMONSTRATION PROGRAM  ON  MARCH
       22.  DURING  THE  REPORT PERIOD,  THE TOTAL SCRUBBER  OUTAGE TIME WAS 0.33 H«.   THE  SYSTEM  HAS
       BEEN IN  SERVICE  ON  A  VIRTUALLY  CONTINUOUS BASIS SINCE OCT. 17,  TOTALLING  OVER  5  MONTHS  OF
       100X RELIABLE OPERATION.

       THE PROGRAM  WAS  TERMINATED TO ALLOW CIC 10 DEVELOPS AND DEMONSTRATE A NEW FGD  DESIGN.
       NO DEMONSTRATION COMMITMENTS  HAVE YET BEEN MADE.
                                                   193

-------
                 TABLE 12
DESCRIPTION OF TERMINATED FGD SYSTEMS   01/78
UTILITY NAME

UNIT NAME

UNIT LOCATION

UNIT RATING

FUEL CHARACTERISTICS

FGD VENDOR

PROCESS

NEW OR RETROFIT

START UP DATE

FGO STATUS

EFFICIENCYr
 PARTICULATES
 ILLINOIS POWER

 WOOD RIVER NO a

 EAST ALTON ILLINOIS

  110 MW

 COAL   2.9-3.2 PERCENT SULFUR

 MONSANTO ENVIRO CHEM SYSTEMS

 CATALYTIC OXIDATION

 RETROFIT

 10/72

 TERMINATED


 99 PERCENT
  S02
                      85 PERCENT
WATER MAKE UP
 SLUDGE  DISPOSAL
                       SULFURIC  ACID  PRODUCT
UNIT  COST
 OPERATIONAL
  EXPERIENCE
SEE APPENDIX A,  FGD SYSTEM ECONOMICS
 REFER TO THE BACKGROUND INFORMATION SECTION IN TABLE 12.  SYSTEM START-UP
 OCCURRED IN OCTOBER 1972.  INITIAL AND SUBSEQUENT OPERATIONS hERE
 ACCOMPANIED BY A NUMBER OF SEVERE MECHANICAL-RELATED PROBLEMS RESULTING
 IN LIMITED OPERATIONS AND EVENTUAL TERMINATION OF THE PROGRAM.  TOTAL
 OPERATION TIMt WAS <444 HOURS IN 1972, 158 HOURS IN 19/3 AND 55 HOURS IN
 1974.
                                             194

-------
                                       BACKGROUND  INFORMATION
                                                 ON
                                          MOOD RIVER NO.  H

     THE  WOOD  RIVER POWER STATION OF THE ILLINOIS  POWER  COMPANY  IS  LOCATED  NEAR  EAST  ALTON,
ILLINOIS,  NORTH  OF  ST.  LOUIS, MISSOURI.  THE NO. 4 BOILER  IS A COMBUSTION ENGINEERING  PULVERIZED-
COAL-FIRED UNIT  THAT  HAS A GROSS RATED CAPACITY OF 109 MW  AND  A  NET CAPACITY  OF  loi MW.   THIS  UNIT
FIRES A HIGH  SULFUR CENTRAL ILLINOIS COAL WITH TYPICAL CHARACTERISTICS  OF 3.1  PERCENT  SuLFUK,  1U
PERCENT ASH AND  A HEAT  CONTENT OF 10,800 BTU/LB.   ANNUAL  COAL  CONSUMPTION IS  APPRUXIMATELY 275,OUO
TONS/YEAR.

     THE  EMISSION CONTROL EQUIPMENT FOR THIS BOILER  INCLUDES MECHANICAL COLLECTORS, A  HIGH EFFIC-
IENCY ESP, AND A MONSANTO CATALYTIC OXIDATION  (CATOX) FGD  SYSTEM FOR THE CONTROL OF PART1CULATEb AND
SULFUR DIOXIDE.   DESI&N REMOVAL EFFICIENCIES UF THIS CONTROL SYSTEM ARE 99.9  PERCENT  FOR  PARTICUL-
ATES AND  85 PERCENT FOR SULFUR DIOXIDE.  INLET SULFUR DIOXIDE  CUNCENTHAT IONS  TO  THE CATuX SYSTEM AWE
GENERALLY IN THE 2000 TO 2200 PPM RANGE.

     FOLLOWING PASSAGE THROUGH THE PARTICULATE REMOVAL SYSTEM, THE  FLUE GAS ENTERING  THfc  SCROBbING
SYSTEM IS HEATED TO A TEMPERATURE OF 850 F  AND PASSES THROUGH  A  VANADIUM PENTOXIDt FIXED-BED  CATALY-
TIC CONVERTER, WHERE THE SULFUR DIOXIDE IS  OXIDIZED  TO SULFUR  THIOXIDE. THE  GAS THEN  FLOWS THROUGH
AN ACID ABSORPTION TOWER, WHERE THE SULFUk  TRIOXIDE  IN THE  GAS IS CONVERTED TO SULFuKIC  ACID.   AN
ACID MIST ELIMINATOR ENSURES REMOVAL OF ENTRAINED  ACID MIST FROM THE GAS STREAM.  THE  CLEANED  GAS IS
DISCHARGED TO THE STACK AND THE PRODUCT ACID IS COOLED AND  STORED IN TANKS.  A SIMPLIFIED PROCF_SS
FLOW DIAGRAM OF THE WOOD RIVER CATOX SYSTEM IS PRESENTED  IN APPENDIX B.

     THIS DEMONSTRATION SYSTEM, PARTIALLY FINANCED BY EPA,  WAS STARTED  UP IN  SEPTEMBER 1972.   WHILE
THE MAIN  PARTS OF THE UNIT PERFORMED ACCEPTABLY, VARIOUS  TROUBLES WITH  ASSOCIATED  EQUIPMENT CAUSED
EXTENSIVE SHUTDOWNS AND DELAYS, TO THE EXTENT  THAT APPROXIMATELY 27 DAYS OF FULL OPERATION HAVE SEEN
OBTAINED   IN ALMOST TWO YEARS.  A d«-HOUR PERFORMANCE TEST  RUN  WAS COMPLETED IN JULY 1973.  THE
FOLLOWING GUARANTEES WERE ACHIEVED AND EXCEEDED:   90 PERCENT CONVERSION OF  SULFUR  DIOXIDE TO  SULFUR
TRIOXIDE   IA80UT 85 PERCENT NET REMOVAL), 99 PERCENT  REMOVAL OF PARTICULATE  ENTERING THE  SYSTEM, LfcSS
THAN  1 MG/ACF OF ACIO MIST IN GAS LEAVING THE  SYSTEM, PRODUCTION OF 60  DEGREES BAUME  ACID.

PERFORMANCE SUMMARY

      THE  WOOD RIVER SYSTEM WAS STARTEO-UP IN SEPTEMBER  1972 BUT  WAS SHUT DOWN  ALMOST  IMMEDIATELY
 (IN  OCTOBER)  TO CONVERT THE  BURNERS TO OIL  FIRING, WHICH  WAS NOT COMPLETED  UNTIL JUNE  1973.   A
SUCCESSFUL PERFORMANCE TEST  WAS THEN MADE,  BUT BECAUSE OF  THE  CATALYST  PLUGGING  HAZARD,THE SYSTEM
MS  SHUT  DOWN AGAIN TO  INSTALL AN EXTkNAL BURNER SYSTEM,  WHICH WAS  NOT  COMPLETED UNTIL APRIL  19M.
VARIOUS  OTHER PROBLEMS WITH  STANDARD EQUIPMENT HAVE  BEEN  ENCOUNTERED SINCE, WITH THE  RESULT THAT
ONLY  b57  HOURS OF OPERATING  TIME HAVE  BEEN  LOGGED  IN TWO  YEARS,

      SEVERAL  OTHER MAJOR PROBLEM AREAS ENCOUNTERED DURING  THE  INTERMITTENT  UPERATION  Of  THIS  REGENE-
RABLE SYSTEM  INCLUDED:  FROZEN DAMPERS ON REHEAT BURNERS,  CRACKS IN THE TEFLON LINEH  UN  THE ACID
PUMP'S DISCHARGE HEADER, CRACKS IN THE REHEAT  DUCTING, FALL OF REFRACTORY BRICKS FROM  THE REHEA1EK
 BURNER DOME,  AND NEED FOR REINFORCEMENT OF  THE STRUCTURE  SUPPORTING THE HIGH  TEMPEKATUR  FLUE  GAS
 DUCT TO  THE CATALYTIC CONVERTER.
                                                   195

-------
ILLINOIS POWtK                          OPEKATING LOG            WOOD RIVER UNIT NO.  4
                                 CATALYTIC OXIDATION SYSTEM
                            WOOD RIVtR NO. 4 - ILLINOIS POWER CO.
                                        1972 TO 1973

     DATE                HOURS                          DATE                 HOURS
   10-6-72                 an                            9-4-72                12
   10-9-73                 en                            9-5-72                2"
  10-10-72                 16                            9-6-72                24
  10-13-72                 20                            9-7-72                 ^
  10-14-72                 16                           9-11-72                 2
  10-30-72                 24                           9-12-72                16
  10-31-72                 16                           9-13-72                24
   7-21-73                 18                           9-14-72                24
   7-22-73                 24                           9-15-72                24
   7-23-73                 18                           9-16-72                24
   7-24-73                 24                           9-17-72                24
   7-2b-73                 14                           9-18-72                24
   7-26-73                 13                           9-19-72                 5
   7-17-73                 19                           9-24-72                17
   7-28-73                 19                           10-6-72                12
   7-29-73                  9                           10-7-72                24

NOTE:  THE OPERATION TIME LOG DOES NOT INCLUDED INTERMITTENT
SYSTEM OPERATION DURING 1974.  SYSTEM OPERATIONS FOR 1974
AMOUNTED TO Sb HRS.  TOTAL OPERATION TIME FOR 2.5 YRS. OF
OPERATION WAS 657 HRS.
                                                  196

-------
                 TABLE 12
DESCRIPTION OF TERMINATED FGD SYSTEMS   01/76
UTILITY NAME

UNIT NAME

UNIT LOCATION

UNIT RATING

FUEL CHARACTERISTICS

FGD VENDOR

PROCESS

NEW OR RETROFIT

START  UP DATE

FGD STATUS

EFFICIENCY,
  PARTICULATES
 KEY  WEST  UTILITY BOARD

 STOCK  ISLAND PLANT

 KEY  WEST  FLORIDA

   37 MW

 OIL  2.4 PERCENT SULFUR

 ZURN AIR  SYSTEMS

 LIMESTONE SCRUBBING

 NEW

 10/72

 TERMINATED


 90 PERCENT
  S02
 WATER  MAKE  UP
 SLUDGE  DISPOSAL
 UNIT  COST
 OPERATIONAL
  EXPERIENCE
                       65  PERCENT-ESTIMATED
                       OPEN  LOOP 2.7  GPM/MW
                       SOLAR  EVAPORATION POND
SEE APPENDIX A, FGO SYSTEM ECONOMICS
 REFER TO BACKGROUND INFORMATION IN TABLE 12 OF THIS REPORT. THIS
 FGD SYSTEM HAS FIRST PLACED IN SERVICE OCTOBER 1972. THE FSO SYSTEM HAS
 BEEN OUT OF SERVICE SINCE JANUARY 28, 1975. EXTENSIVE MODIFICATIONS AND
 REPAIRS HAVE BEEN REQUIRED.  RESUMPTION OF OPERATIONS IN THE FUTURE
 LOOKS VERY DOUBTFUL.
                                              197

-------
                                       BACKGROUND  INFORMATION
                                                 ON
                                         STOCK ISLAND PLANT

     THE UTILITY BOARD OF THE CITY OF KEY WEST OWNS AND OPERATES  A NEW  37-MW  OIL-FIRED POWER BOILER,
INSTALLED AT THEIR STOCK ISLAND PLANT WHICH IS LOCATED DIRECTLY ADJACENT  TO THE  ISLAND CITY OF KEY
WEST.  THE BOILER IS AN ERIE CITY BALANCED-DRAFT OIL-FIRED UNIT THAT  IS NOMINALLY  RATED AT 37 Mw AND
CAN ACHIEVE 42 MW AT FULL PERFORMANCE.  THE UNIT FIKES NO. 6 RESIDUAL FUEL OIL FROM VENEZUELA WITH
SULFUR AND ASH CONTENTS OF 2.75 AND 0.05 PERCtNT,  RESPECTIVELY.   THE  UNIT'S GROSS  HEAT RATE IS
11,380 BTU/KWH.  INITIAL OPERATION OF THE UNIT COMMENCED IN NOVEMBER  1973.

     THE EMISSION CONTROL SYSTEM FOR THIS UNIT CONSISTS OF A MULTIPLE TUBE MECHANICAL  OUST COLLECTOR
INSTALLED UPSTREAM OF TWO SULFUR DIOXIDE WET SCRUBBERS DESIGNED AND INSTALLED BY ZURN  AIR INDUS-
TRIES.  THIS IS A DEMONSTRATION FACILITY CEPA FUNDED) EMPLOYING LIMESTONE  IN  A SEAWATER SOLUTION FOK
THE REMOVAL OF SULFUR DIOXIDE FROM THE BOILER FLUE GAS STREAM.  NO PROVISIONS FOR  STACK GAS REHEAT
EXIST AT THE FACILITY.

     THE LIMESTONE ABSORBENT IS OBTAINED FROM CORAL DREDGED FROM  THE  OCEAN.   THE CORAL CONSISTS
PRIMARILY OF CAC03 WITH LITTLE OR NO MGC03.  THE CORAL IS GROUND  TO A FINE POWDER  IN A HAMMERMlLL
CRUSHER TO 90 PERCENT MINUS 325 MESH AND SLURRIED  IN SEAWATEK.

     ZURN DUSTRAXTORS ARE EMPLOYED FOR THE REMOVAL OF SULFUR UIOXIOE  AND  RESIDUAL  PARTICULATE FROM
THE BOILER FLUE GAS.  THE TrtO SCRUBBER MODULES ARE DESIGNED TO HANDLE A COMBINED TOTAL OF 126,950
CFM AT 150 F.  FLUE GASES FROM THE BOILER ARE DRAWN THROUGH AN INDUCED DRAFT FAN AND FORCED EITHER
THROUGH THE BYPASS DUCT OR THROUGH ONE OR BOTH SCRUBBERS VIA THREE SETS OF DAMPERS  BETWEEN THE
INDUCED-DRAFT FAN AND THE STACK.  BEFORE ENTERING  THE SCRUBBING SYSTEM THE GAS is  COOLED  FROM 360  F
TO 160 F BY SEAWATER SPRAYS.  THIS COOLING PROTECTS THE FIBERGLASS COMPONENTS OF THE SCRUBBER
MODULES.  A PRESSURE DROP OF 12 TO It INCHES WATER GAUGE IS THE NORMAL OPERATING RANGE FOR THE
SCRUBBERS.  THE SPENT SCRUBBING SLURRY IS BLED OFF TO TWO ON-SITE SETTLING PONDS WITH  A RETENTION
CAPACITY OF 21 DAYS.  THE SLUDGE SETTLES OUT AND CLARIFIED WATER  IS DISCHARGED BACK  INTO  THE  SEA BY
AN OVERFLOW PIPE AND SEEPAGE.  THE PARTICULATE AND SULFUR DIOXIDE REMOVAL EFFICIENCIES UF THE
EMISSION CONTROL SYSTEM ARE 64 TO 82 PERCENT AND 68 TO 73 PERCENT, RESPECTIVELY.   ACTUAL  INLET AND
OUTLET SULFUR DIOXIDE LOADINGS ARE 1300 TO 1500 PPM AND 300 TO 500 PPM.   INLET AND  OUTLET PARTICU-
LATE LOADINGS ARE 0.20 GR/SCF AND 0.05 GR/SCF.

SYSTEM PERFORMANCE

     START-UP OF THE SCRUBBING SYSTEM OCCURRED IN  AUGUST 1973.  ENSUING OPERATION  HAS  PROCEEDED  UN
AN INTERMITTENT BASIS.  THE MAJOR PROBLEM AREAS ENCOUNTERED HAVE  INCLUDED:
    •SEVERE CORROSION OF GAS UUENCH DUCT AND DAMPER SfcALIuG FANS  ON INLET AND OUTLET OF SCRUBBERS.
    •PLUGGING AT THE BOTTOM OF SCRUBBER TUBES.
    •LIUUIO LEVEL CONTROL FAILURES IN THE SCRUBBER MODULES.
    •POOR LIMESTONE UTILIZATION (APPROXIMATELY 20  PERCENT).
    •INDUCED DRAFT FAN REPAIRS.
    •REPLACEMENT OF INTERNAL STAINLESS STEEL PARTS WITH MONEL COMPONENTS.
    •BOILER FOUNDATION AND BOILER TUBE PROBLEMS.
    •LIMESTONE SUPPLY SHORTAGES.

     ADDITIONAL INFORMATION AND DETAILS ON THE PROGRESS OF THIS INSTALLATION ARE PRESENTED IN THE
PERFORMANCE TABLE BELOW.  A PROCESS FLOW DIAGRAM IS PRESENTED IN  APPENDIX B.
                                                 198

-------
KEY  WEST  UTILITY BOARD
                                                           STOCK ISLAND PLANT
PERIOD TOTAL P
SEP-
OCT.
NOV.
DEC.
JAN.
FEB.
MAR.
APR.
MAY
JUN.
JUL.
AUG.
SEP.
OCT.
NOV.
OEC.
JAN.
FEB.
MAR.
APR.
MAY
JUN.
JUL.
AUG.
AUG.
SEP.
OCT.
NOV.
DEC.
JAN.
FES.
MAR.
APR.
MAY
JUN.
JUL.
AUG.
TOTAL
72
72
72
72
73
73
73
73
73
73
73
73
73
73
73
73
74
74
74
74
74
74
74
74
74
74
74
74
74
75
75
75
75
75
75
75
75

696
744
720
744
744
672
744
720
744
720
744
744
720
744
720
744
744
672
744
720
744
720
744
552
840
672
672
840
672
672
840
672
672
840
672
672
840
26680
BOILER
      0
      0
    528
    192
    384
    672
    744
    720
    744
    720
    744
    744
    720
    522
    720
    744
    624
    600
    744
    720
     30
    120
    744
    552
    641
     36
    672
    840
    672
    672
    642
    672
    672
    840
    672
    672
    IbO
   20895
AS OF MARCH 1977  IT HAD NOT BEEN DECIDED
WHETHER  THERE WOULD BE FUTURE FGO OPERA-
TIONS AT THE STOCK ISLAND PLANT.
                                                          0
                                                          0
                                                          0
                                                          0
                                                          0
                                                        120
                                                          0
                                                          0
                                                          0
                                                          0
                                                          0
                                                         40
                                                          0
                                                         24
                                                         42
                                                         72
                                                        209
                                                          0
                                                          0
                                                          0
                                                          0
                                                          0
                                                          0
                                                         24
                                                        216
                                                          0
                                                        252
                                                        362
                                                        108
                                                        110
                                                          0
                                                          0
                                                          0
                                                          0
                                                          0
                                                          0
                                                          0
                                                       1579
                                                             ,HRS)
OPERAblLITY
      0
      0
      0
      0
      0
     18
      0
      0
      0
      0
      0
      5
      0
      5
      6
     10
     33
      0
      0
      0
      0
      0
      0
      4
     34
      0
     38
     43
     16
     16
      0
      0
      0
      0
      0
      0
      0
      8
                                                                                   U)
                                                199

-------
                 TABLE 12
DESCRIPTION OF TERMINATED FGO SYSTEMS  01/78
UTILITY NAME


UNIT NAME


UNIT LOCATION


UNIT RATING


FUEL CHARACTERISTICS


FGO VENDOR


PROCESS


NEW OR RETROFIT


START UP DATE


FliD STATUS


EFFICIENCY,
 PARTICULATES
POTOMAC ELECTRIC & POWER

DICKERSON NO. 3


OICKERSON MARYLAND


  95 MW

COAL   2.U PERCENT SULFUR

CHEMICO

MAGNESIUM OXIDE SCRUBBING

RETROFIT


 9/73

TERMINATED



99.3 PERCENT
 SU2
                      90 PERCENT
MATER MAKE UP
3.2 GPM/MW
SLUDGE DISPOSAL
                      ACID PLANT REGENERATION
 UNIT  COST
                      SEE  APPENDIX A, FGO SYSTEM ECONOMICS
 OPERATIONAL
  EXPERIENCE
REFER TO BACKGROUND INFORMATION SECTION IN TABLE 12 OF THIS REPuRT.
A SINGLE, TWO-STAGE VENTURI SCRUBBER-ABSORBER MODULE UTILIZING  THE
CHEMICO-BASIC MAGNESIUM OXIDE SULFUR DIOXIDE REMOVAL/RECOVERY PROCESS
WAS RETROFITTED ONTO THE NO. 3 UNIT, HANDLING APPROXIMATELY 50  PERCENT
OF THE COAL-FIREO FLUE GAS. THE MAGNESIUM SULFITE BY PRODUCT WAS REGEN-
ERATED AT AN EPA-FINANCED REGENERATION FACILITY AT THE ESSEX CHEMICAL
COMPANY IN RHODE ISLAND. MAGOX OPERATIONS WERE COMPLETED  IN 08/75.
PARTICULATE MODE OPERATIONS ARE CONTINUING.
                                             200

-------
                                       BACKGROUND  INFORMATION
                                                 ON
                                         DICKERSON NO.  3

     THE  DICKERSON STATION OF POTOMAC ELECTRIC POWER  CO.  (PEPCO)  IS  LOCATED  ON  THE  POTOMAC  RIVER
NEAR  OICKERSON,  MARYLAND, ABOUT 30 MILES NORTHWEST OF  WASHINGTON,  D.C.   THE  STATION HAS  3 ELECTRIC
GENERATORS,  EACH RATED AT 190 MN.  UNIT NO.  3  IS A DRY  BOTTOM  COAL-FIRED  BOILER  DESIGNED BY  COMBUS-
TION  ENGINEERING AND INSTALLED IN 1962.  THE COAL  NOW  BURNEU HAS  AN  AVERAGE  GROSS HEATING VALUE OF
11,700  BTU/LB AND AVERAGE ASH AND SULFUR CONTENTS  OF  It AND 2  PERCENT,  RESPECTIVELY.   TH£ 60ILER  IS
FITTED  WITH  AN ELECTROSTATIC PRECIPITATOR DESIGNED AND  INSTALLED  BY  RESEAKCH-COTTfiELL  IN 1962.  THE
FGD SYSTEM EMPLOYS THE CHEM1CO-6ASIC MAGNESIUM OXIDE  SCRUBBING PROCESS.   THE RETROFIT  SYSTEM HANDLES
APPROXIMATELY 50 PERCENT OF THE EXHAUST GAS  FROM THE  NO.  3 UNIT.

     THE  FGD SYSTEM CONSISTS OF A SINGLE, TWO-STAGE SCRUBBER/ABSORBER,  WHICH INCORPORATES AN ADJUST-
ABLE-THROAT  VENTURI SCRUBBER FOR PART1CULATE REMOVAL  AND  A SECOND STAGE  ABSORBER WITH  A  FIXED
VENTURI TO REMOVE SULFUR DIOXIDE.  THE LIQUOR  STREAMS FOR BOTH STAGES  ARE SEPARATE  AND OPERATE  IN  A
CLOSED-LOOP  MODE.  UNTIL MID-1975 THE MAGNESIUM  SULFITE GENERATED WAS  TRANSFERRED TO AN  EPA  FINANCED
FACILITY  AT  THE ESSEX CHEMICAL COMPANY SULFURIC  ACID  MANUFACTURING PLANT  IN  RUMFORD, RHODE  ISLAND,
WHERE MAGNESIUM OXIDE WAS REGENERATED AND SULFUR DIOXIDE  FROM  THE REGENERATION  PROCESS WAS  CONVERTED
TO SULFURIC  ACID.  THE RUMFORD FACILITY HAS  SINCE  BEEN CLOSED  DOWN.   A  GENERAL  PROCESS FLOW  DIAGRAM
OF THE DICKERSON NO. 3 WET SCRUBBING SYSTEM  AND  REGENERATION FACILITIES  IS PRESENTED IN  APPENDIX  B.

     CONSTRUCTION WAS COMPLETED  IN AUGUST AND  THE  SYSTEM  STARTED  UP  IN  SEPTEMBER 1973.  DURING
INTERMITTENT OPERATIONS  FOR  SHAKEDOWN THROUGH  JANUARY 197
-------
POTOMAC ELECTRIC » POWER       FGD SYSTEM OPERATING HISTORY       DICKERSON  UNIT  NO. 3

OPERATING PERIOD                              COMMENTS
SEP. 73    PROBLEMS DURING THIS PERIOD RANGED FROM CORROSION  LEAKS  IN  EXPANSION  JOINTS TO PROBLEMS
  TO       IN MATERIAL HANDLING EQUIPMENT, FEEDING AND SLAKING OF MGO,  PLUGGING  IN THE MGO MIX TANK
JAN. 74    AND SUCTION LINES TO THE MGO MAKE-UP PUMPS.

JAN. 74    MAINTENANCE AND MODIFICATIONS WERE PERFORMED ON THE SYSTEM.   THE  MAJOR  SYSTEM REVISION
  TO       MADE DURING THIS PERIOD WAS THE ADDITION OF A PRE-MIX  TANK  IN  THE MGO SYSTEM.
APR. 74

APR. 74    LIMITED OPERATION BECAUSE THE UTILITY DID NOT HAVE ACCESS TO  THE  EPA  CALCINING FACILITY
  TO       AT THE ESSEX CHEMICAL COMPANY SULFURIC ACID PLANT.  BY THE  END OF  JUNE  1974,  ALL  THE
JUL. 74    MGO AT DICKERSON HAD BEEN USED AND A SILO PLUS THREE CARS WERE FULL OF  MGS03.

AUG. 74    DURING THIS PERIOD THE SYSTEM GENERALLY OPERATED AT 75 PERCENT OF  THE DESIGN  GAS  FLOW.
  TO
DEC. 74

JAN. 75    PROBLEMS DEVELOPED IN THE BUCKET ELEVATOR TRANSPORTING THE  MGS03  FROM THE  DRYER TO  THE
FEB. 75    STORAGE SILO.  UNIT NO. 3 WAS TAKEN OUT OF SERVICE FOR AN 8  TO 12  WEEK  TURBINE OVERHAUL.
  TO       THE SCRUBBER WAS INSPECTED, MAINTENANCE AND MODIFICATIONS WERE MADE.
JUL. 75

AUG. 75    THE FGD SYSTEM WAS RESTARTED IN AUGUST.  STEAM WAS LOST TO  THE MGO MIX  TANKr  RESULTING
           IN A VERY MOIST PRODUCT FROM THE CENTRIFUGE.  CAKING IN THE DRYER  OCCURRED.   AT THIS
           POINT, THE UTILITY DECIDED TO TEST ONLY THE FIRST-STAGE OF  THE SCRUBBING SYSTEM,  TAKING
           GAS AHEAD OF THE PRECIPITATOR.  FGO OPERATION AT DICKERSON  TERMINATED AT THIS POINT.
                                                 202

-------
                 TABLE  12
DESCRIPTION OF TERMINATED  FGD  SYSTEMS   01/76
UTILITY NAME          PUBLIC  SERVICE  CO OF COLORADO

UNIT NAME             VALMONT  NO.  5

UNIT LOCATION         VALMONT  COLORADO

UNIT RATING              50  Mh

FUEL CHARACTERISTICS  COAL  0.72 PERCENT SULFUR

FGD VENDOR            UOP/PUB  SERVICE OF COLORADO

PROCESS               LIMESTONE SCRUBBING

NEW OR RETROFIT       RETROFIT

START UP DATE         10/74

FGD STATUS            TERMINATED

EFFICIENCY,
  PARTICULATES         95 PERCENT


  802                  65 PERCENT


WATER MAKE  UP         CLOSED  LOOP


SLUDGE DISPOSAL


UNIT COST


OPERATIONAL           REFER TO BACKGROUND INFORMATION IN TAbLE 12 OF  THIS REPORT.  THIS FGO
  EXPERIENCE           SYSTEM  HAS BEEN OPERATIONAL SINCE NOVEMBER 197
-------
                                       BACKGROUND INFORMATION
                                                 ON
                                           VALMONT NO. 5

     THt VALMONT POWER STATION OF THE PUBLIC SERVICE OF COLORADO  IS LOCATED  IN  VALMONT  (NEAR
BOULDER, COLO.), COLORADO, APPROXIMATELY SO MILES NORTH Of DENVER.  VALMONT  NO.  5  IS  A  166 MW (SOd
SCRUBBING CAPACITY-50 MW MOOULE) PULVERI ZED-COAL FIRED UNIT.  VALMONT NO.  5  CAME ON LINE  ORIGINALLY
IN i<>64 AND EMPLOYS A ONCE-THROUGH COOLING SYSTEM UTILIZING RESERVOIRS TOTALING  APPROXIMATELY 530
SURFACE ACRES.  THE STATION BURNS A WYOMING ROSEBUD SUB-BITUMINOUS TYPE COAL  WITH  A SULFUR CONTENT
OF APPROXIMATELY 0.6 PERCENT, AN ASH CONTENT OF 5.2 PERCENT, AND  A CALCIUM OXIDE CONTENT  OF APPROX-
IMATELY 2U PERCENT IN THE FLYASH.  THE ORIGINAL AIR QUALITY CONTROL EQUIPMENT AT THE  PLANT CONSIST-
ED OF A MECHANICAL COLLECTOR FOLLOWED IN SERIES BY A COLD SIDE ESP.  PUBLIC  SERVICE COMPANY OF
COLORADO LATER EQUIPPED FIVE BOILERS WITH UNIVERSAL OIL PRODUCTS  (UOP) TCA WET  PAHTICULATE
SCRUBBERS.  EACH OF THE TURBULENT CONTACT ABSORBERS (TCA) CONSISTS OF THREE  STAGES OF PLASTIC MOBILE
PACKING SIMILAR TO "PING PONG" BALLS, WITH A WATER SPRAY DIRECTED DOWNWARD THROUGH THE  PACKING
COUNTER CURRENT TO THE FLUE GAS FLOW.  AT VALMONT NO. 5 ALL OF THE FLUE GASES PASS THROUGH A MECH-
ANICAL COLLECTOR AFTER WHICH THEY ARE DIVIDED, WITH APPROXIMATELY 50 PERCENT  OF  THE GAS FLOW GOING
TO THE PRECIPITATOR AND THE OTHER 50 PERCENT TO THE 2 MODULE SCRUBBER.  AFTER EXITING THE  ESP AND
SCRUBBER, THE GAS FLOWS ARE JOINED TOGETHER AND DISCHARGED SIMULTANEOUSLY  TO  THE STACK.

     ALTHOUGH THE SCRUBBER WAS ORIGINALLY INSTALLED SPECIFICALLY  FOR PARTICULATE REMOVALi  SINCE  THE
PLANT BURNS LOW SULFUR COAL, 45 PERCENT OF THE SOS WAS REMOVED AS WELL BECAUSE  OF  THE ALKALINITY OF
THE FLYASH.

     DURING THE FIRST YEAR OF OPERATION PROBLEMS INCLUDED DIFFICULTIES WITH  THE MODULE  PACKING GRID
SUPPORT, GENERAL VESSEL SCALE FORMATION, FLOW DISTRIBUTION PROBLEMS, BALL  BREAKAGE, SCALING IN THE
MIST ELIMINATOR SECTION, AND PLUGGING OF THE REHEATER.  SCALE FORMATION WAS  THE MOST  PREDOMINANT
CONTINUING MAJOR CAUSE OF DOWNTIME IN THE SCRUBBER.  SCALE ACCUMULATION WAS  NOTED ON  THE  WET-DRY
INTERFACE IMMEDIATELY DOWNSTREAM OF THE PRESATURATION NOZZLES.  SCALE ALSO ACCUMULATED  HEAVILY ON
THE UNDERSIDE OF THE FIRST LAYER OF GRID BARS.

     SCALE ON THE UPPER GRID BARS WAS LESS PREVALENT AS THE ACTION OF THE  "PING PONG" BALLS TENDS  TO
KEEP THE SCALE  OFF OF THESE SECTIONS.  SCALE ALSO COLLECTED ON THE WALLS OF  THE VESSEL  AND INTER-
MITTENTLY SLOUGHED OFF AND FELL INTO THE SUMP IN LARGE PIECES CAUSING BLOCKAGE OF  THE RECIRCULATION
PUMP SUCTION SCREENS.  SCALING OF THE MIST ELIMINATOR ABATED SOMEWHAT WITH THE  INTRODUCTION OF A
CLEAR RINSE WATER WASH.  SCALt FORMATION IN THE REHEAT SECTION SOMETIMES REQUIRED SUPPLEMENTAL
CLEANING OF THE REHEATER IN ADDITION TO THE CLEANING OBTAINED BY  THE USE OF  THE SOOT8LOWERS WHICH
WERE INSTALLED  AS PART OF THE REHEATER EQUIPMENT.  UNDER NORMAL OPERATION, THE  SOOTBLOWERS LOCATED
IN THIS REHEAT  SECTION WERE FAIRLY SUCCESSFUL IN REMOVING THE ACCUMULATION OF THE SCALE IN THE
REHEATER.

     ALTHOUGH MANY OF THE INITIAL START-UP PROBLEMS WERE SOLVED OVER A PERIOD OF TIME,  THE CALCIUM
SULFATE-FLY ASH SCALING CONTINUED TO BE A SIGNIFICANT OPERATING PROBLEM AT THE  VALMONT  INSTALLATION,
IN ADDITION TO  THESE SCALING RELIABILITY PROBLEMS, A WATER QUALITY CONCERN ALSO SURFACED  THAT WAS  A
DIRECT  RESULT OF THE PARTICULATE SCRUBBER OPERATION.  THE RELATIVELY HIGH  CAO CONCENTRATION IN THE
VALMDNT FLY ASH RESULTED IN FAIRLY HIGH S02 REMOVAL RATES (05-50  PERCENT)  WITHIN THE  UNITS.  SINCE
NO PH CONTROL CAPABILITY FOR EITHER THE RECIRCULATING SLURRY OR THE SYSTEM SLOWDOWN SLURRY WAS
DESIGNED INTO THE SYSTEM, AN ACID CONDITION WAS CREATED IN THE SLURRY AND  THE SLOWDOWN  STREAM.
PH LEVELS OF THE BLOWDOWN NORMALLY RANGED BETWEEN 1.7 AND 2.0.  ALTHOUGH THE  STREAM WAS NEUTRALIZED
TO A DEGREE BY  ALKALINE FLY ASH, PSCC FELT THAT IT WAS IMPORTANT  TO INVESTIGATE VARIOUS CONTROL
MEASURES WHICH  COULD BE APPLIED TO THIS STREAM.  THE CALCIUM SULFATE SCALING  PROBLEM  WAS  THOUGHT TO
BE THE  RESULT OF A SUPER-SATURATED CALCIUM SULFATE CONDITION IN THE RECIRCULATING  SLURRY.   BECAUSE
OF THIS  IT WAS  FELT THAT CONTINUOUS PH CONTROL OF THE RECIRCULATING SLURRY,  CONVERSION  OF  THE SYSTEM
TO CLOSED LOOP  OPERATION AND ESTABLISHING A HIGHER CONCENTRATION  OF SEEDING  SOLIDS IN THE  RECIRCULA-
TION SLURRY (THEREBY CONTROLLING THE SCALING PROBLEMS WITHOUT CHEMICAL ADDITIVES)  WOULD BE NECESSARY
MEASURES.

     FOR PH CONTROL, LIMESTONE WAS TESTED INITIALLY, THEN LIME WAS UTILIZED  FOR  THE ALKALI REAGENT.
IN THE  FIRST TEST, SINCE LIMESTONE UTILIZATION WAS A MAJOR CONCERN, A SPECIAL EFFORT  WAS  MADE TO
REDUCE  THE POTENTIAL FOR THE SHORT CIRCUITING OF THE ADDED LIMESTONE AND TO  PROVIDE SUFFICIENT
RESIDENCE TIME  IN THE REACTOR SECTION OF THE SYSTEM.  6Y UTILIZING FOUR REACTION MIX  TANKS IN
SERIES, PLUG FLOW WAS EXPECTED TO BE MORE CLOSELY SIMULATED.  TO  MAINTAIN  A  CLOSED LOOP SYSTEM WHtRE
THE QUANTITY OF WATER REMOVED FROM THE SYSTEM WAS HELD TO A MINIMUM, FOUR  SYSTEM DESIGN FEATURES
WERE UTILIZED.
     1. UTILIZATION OF A COMBINATION OF POND SUPERNATANT AND MAKE-UP WATER FOR  RECYCLE  WATER.
     2. PRESATURATION OF THE INCOMING FLUE GAS WITH RECIRCULATING SLURRY.
     3.  INTERMITTENT MIST ELIMINATOR WASH,
     4. PROPER  SELECTION OF MATERIALS OF CONSTRUCTION TO PROTECT  AGAINST ATTACK  CAUSED  BY  HIGH
        CHLORIDE CONCENTRATIONS.

     THE SCRUBBERS R & D FACILITY WAS NOT EQUIPPED WITH A MECHANICAL THICKENER  FOR CONTROL OF THE
SUSPENDED SOLIDS CONCENTRATION OF THE RECIRCULATING SLURRY  (ALL PURGED MATERIAL  WAS SENT  TO THE
SLUDGE  POND).   WITH A 500 PPM S02 CONCENTRATION IN THE FLUE GAS,  IT IS EXPECTED  THAT  THE  RECIRCULAT-
ING SLURRY SOLIDS COULD BE REALLY CONTROLLED IN THE S TO 7 PERCENT RANGE.  DUE  TO  THE MIXED FUEL
FIRED AT THE UNIT DURING THE TEST PERIOD, HOWEVER, THE S02 CONCENTRATIONS  EMITTED  FROM  THE BOILER
AND HENCE PRESENT IN THE FLUE GAS STREAM VARIED SIGNIFICANTLY AND FINALLY  FELL  TO  SUCH  LOW LEVELS
(OFTEN  100-200  PPM) THAT SUSPENDED SOLIDS CONCENTRATIONS IN THE SLURRY COULD .NOT BE MAINTAINED.
IT IS ALMOST CERTAIN THAT A THICKENER, WITH THE SUBSEQUENT RETURN OF SOLIDS  TO  THE SCRUBBER LIQUOH,
COULD HAVE BEEN USED TO GOOD ADVANTAGE DURING THIS TIME PERIOD.   GENERALLY SPEAKING,  THE  SEVERE
SCALING CONDITIONS PLAGUING THE TEST MODULE WERE INTENSIFIED DURING THESE  PERIODS  OF  LOW  INLET  802
CONDITIONS.



                                                 204

-------
                 TABLE  18
DESCRIPTION OF TERMINATED FGO  SYSTEMS   01/78
UTILITY NAME

UNIT NAME

UNIT LOCATION

UNIT RATING

FUEL CHARACTERISTICS

FGD VENDOR

PROCESS

NEW OR RETROFIT

START UP DATE

FGD STATUS

EFFICIENCY,
 PARTICULATES
SOUTHERN CALIFORNIA EDISON

MOHAVE NO 1A

LAUGHLIN NEVADA

 170 MW

COAL  0.5 - 0.8 PERCENT SULFUR

UNIVERSAL OIL PRODUCTS

LIMESTONE SCRUBBING

RETROFIT

11/74

TERMINATED


93 PERCENT
                       95  PERCENT
 WATER MAKE UP
                       0.92  GPM/MW
 SLUDGE DISPOSAL
EXPERIMENTAL METHODS
 UNIT COST
                      NOT  AVAILABLE
 OPERATIONAL
  EXPERIENCE
THIS EXPERIMENTAL MODULE  (VERTICAL TCA TOWER SUPPLIED BY UOP) STARTED up
OCT. 31,  197« AND OPERATED KITH AN AVAILABILITY OF 72X THROUGH 8 MONTHS
OF TESTING, TESTING HAS BEEN COMPLETED, AND THE FGD SYSTEM WAS SHUT DOWN
INDEFINITELY ON JULY 2, 1975. NEVADA ASSEMBLY BILL NO. 706 HAS PLACED A
TWO YEAR  MORATORIUM ON THE ENFORCEMENT OF THE COMPLIANCE SCHEDULE FQK THIS
STATION.  FURTHER FGD ACTIVITIES WILL BE DEPENDENT ON FUTURE LEGISLATION.
                                             205

-------
                 TABLE 12
DESCRIPTION OF TERMINATED F6D SYSTEMS
                                       01/78
UTILITY NAME


UNIT NAME


UNIT LOCATION


UNIT RATING


FUEL CHARACTERISTICS


FGD VENDOR


PROCESS


NEW OR RETROFIT


START UP DATE


FGD STATUS


EFFICIENCY,
  PARTICULATES
SOUTHERN CALIFORNIA EDISON


MOHAVE NO. 3A


LAUGHLIN NEVADA


 160 MM


COAL  0.5-0.8 PERCENT SULFUR


SCE/STEARNS ROGER


LIME SCRUBBING


RETROFIT


11/73


TERMINATED



93 PERCENT
  S02
                      95 PERCENT
 MATER MAKE  UP
                       1.0 GPM/MW
 SLUDGE  DISPOSAL
 UNIT  COST
                      NOT  AVAILABLE
 OPERATIONAL
  EXPERIENCE
REFER TO TH£R BACKGROUND INFORMATION SECTION IN TABLE \i OF THIS REPORT A
PROTOTYPE HOIZONTAL SPRAY TOWER WAS FITTED ONTO THE NO. 2 UNIT AT THIS
STATION AND WAS OPERATED IN AN EXPERIMENTAL MODE FROM JAN. 16, 197« TO
FEB. 9, 1975. SOZ AND PARTICULATE REMOVAL EFFICIENCIES IN EXCESS OF 90X
WERE ACHIEVED DURING THE PROGRAM. FOLLOWING TERMINATION OF THE PROGRAM.
THE MODULE WAS SHUT DOWN, DISASSEMBLED AND SHIPPED TO THE FOUR CORNERS
STATION FOR FURTHER EVALUATION.
                                             206

-------
                                        BACKGROUND INFORMATION
                                                  ON
                          THE MOHAVE  TEST  MODULES PROGRAM:   NOS. 1A AND 2A

     TWO  PHOTOTYPE SULFUR DIOXIDE  ABSORBER MODULES WERE INSTALLED IN 1973 AT THE MOHAVE GENERATING
STATION  OF  THE SOUTHERN CALIFORNIA  EDISON  COMPANY.  A VERTICAL MODULE,  HATED AT 170 Mw, HAS INSTALL-
ED TO TREAT 4bO,000 SCFM PORTION OF  THE FLUE  GAb FROM UNIT  NO. 1.  A HORIZONTAL MODULE, ALSO RATED
JT 170 MW.  WAS INSTALLED TO TREAT  A  SIMILAR FLUE GAS PORTION FRUM UNIT  NO. 2.  UNITS 1  AND 2 ARE
IDENTICAL BOILERS, EACH HAVING  A MAXIMUM NET  CONTINUOUS GENERATING CAPACITY OF 790 MW AND EACH BURN-
ING A WESTERN, LOW-SULFUR COAL  WITH  A  HEATING VALUE OF 11,500 BTU/LB AND ASH AND SULFUR CONTENTS  OF
10 AND 0.1  PERCENT RESPECTIVELY.

VERTICAL MODULE

     THE VERTICAL MODULE, A UNIVERSAL  OIL  PRODUCTS TURBULENT CONTACT ABSORBER (TCA), WAS TESTED IN
TWO MOOES;   FIRST, AS A TCA UNIT,  FROM NOVEMBER 2, 1974 TO  APRIL 30, 1975, AND SECOND AS A POLVGWID
PACKED ABSORBER CPPA), WHEN THE "PING  PONG BALLS" WERE REPLACED WITH A  PLASTIC "EGGCRATE" PACKING
WITH TESTING CONTINUING TO JULY a,  1975.

     STARTUP OF THE VERTICAL  MODULE  WAS INITIATED ON SCHEDULE JANUARY 1, 197fl.  ON JANUARY £«, 1971,
A FIRE BURNED MOST Of THE CHLOROBUTYL  LINING AND SYSTEM RESTART WAS DELAYED UNTIL OCTOBER 1, 1971.
TESTING OF THIS MODULE FOLLOWED A  MONTH LATER AND WAS COMPLETED AFTER 3,131 HRS. OF OP.  THE MODULE
IS PRESENTLY SHUT DOWN IN A COLD STAND-BY  CONDITION AT THE  MOHAVE GENERATING STA.
HORIZONTAL MODULE

     THE HORIZONTAL MODULE, A FOUR-STAGE HORIZONTAL CROSSFLOW SPRAY SCRUBBER, WAS OPERATED 8Y THE
UTILITY IN A SHORT SERIES OF  STARTUP TESTS THAT ENDED ON JANUARY 16, 1971, WHEN A FORMAL TEST PROG-
RAM  WAS INITIATED TO  ASSESS THE PERFORMANCE AND RELIABILITY CHARACTERISTICS OF THE SCRUBBING SYSTEM.
THE  TEST PROGRAM  WAS  TERMINATED ON FEBRUARY 9, 1975 FOLLOWING 5,927 HUURS OF OPERATION.
THE  MODULE WAS SUBSEQUENTLY DISMANTLED, TRANSPORTED, AND REASSEMBLED AT THE FOUR CORNERS PLANT OF
ARIZONA PUBLIC SERVICE WHERE  ADDITIONAL TESTING WAS CONDUCTED AND COMPLETED (DECEMBER 197b).

      INFORMATION  AND  DATA CONCERNING THE PERFORMANCE OF MOHAVE TEST MODULES ARE GIVEN IN THE FOLLOW-
 ING  PERFORMANCE TABLES.   PROCESS FLOW DIAGRAMS OF THE TEST  MODULES ARE  PROVIDED IN APPENDIX B.
                                                  207

-------
SOUTHERN CALIFORNIA EDISON                  MOHAVE UNIT NOS. 1A AND 2A

                                MOHAVE NO. 1A - VERTICAL TEST MODULE
                       OUTAGE TIME HISTORY:  NOVEMBER 2, 1
-------
SOUTHERN  CALIFORNIA EOISON                  MOHAVE UNIT NOS. 1A AND 2A

                               MOHAVE NO. 2A - HORIZONTAL TEST MODULE
                       OUTAGE TIME HISTORY:  JANUARY 16, 1974 TO FEBRUARY 9,  1975

                REASON                                  TIME (HR)
 1.  MODIFY AND REPRIR PLASTIC OEMISTER BLADES             503
 2,  CORRECT BOOSTER FAN BALANCE PROBLEMS                  317
 3.  PUMP REPAIR                                           356
 4.  SPRAY NOZZLE REPLACEMENT                              238
 5.  MODIFY GAS INLET FLOW DISTRIBUTION                    162
 6.  REPAIR HOPPER LEAKS                                   135
 7.  REMOVE HARDHAT FROM THICKENER                          82
 8.  MODIFY SLAKING WATER FOR SCALE PREVENTION              45
 9.  CONDUCT INSPECTION FOR EXTENDED OPERATIONS             19
 10.  TOTAL OUTAGE TIME                                    1757
     TOTAL OUTAGE TIME:  1757 HOURS
     TOTAL CALENDER TIME:   9328 HOURS
     TOTAL OPERATING TIME:  7571 HOURS
     PERCENT AVAILABILITY:  B1.16X
                                                  209

-------
                 TABLE 12
DtSCRIPTION OF TERMINATED F6D SYSTEMS
                                       01/78
UTILITY NAME


UNIT NAME


UNIT LOCATION


UNIT RATING


FUEL CHARACTERISTICS


FGD VENDOR


PROCESS


NEW OR RETROFIT


START UP DATE


FGD STATUS


EFFICIENCY,
  PARTICULATES
TENNESSEE VALLEY AUTHORITY


SHAWNEE NO.  IOC


PAOUCAH KENTUCKY


  10 MW


COAL 2.9 PERCENT SULFUR


TENNESSEE VALLEY AUTHORITY


LIME/LIMESTONE SCRUBBING


RETROFIT
TERMINATED
EXPERIMENTALLY CONTROLLED
  S02
                      EXPERIMENTALLY CONTROLLED
 WATER  MAKE  UP
                      EXPERIMENTALLY CONTROLLED
 SLUDGE  DISPOSAL
                      EXPERIMENTALLY CONTROLLED
 UNIT  COST
                     NOT  APPLICABLE
 OPERATIONAL
  EXPERIENCE
REFER TO BACKGROUND INFORMATION SECTION IN TABLE 12.  THIS EXPERIMENTAL
FGD UNIT BECAME OPERATIONAL IN APRIL, 1972. THE MARBLE-BED ABSORBER, A
30,000 ACF UNIT (10 MW), MANUFACTURED BY COMBUSTION ENGINEERING CO., WAS
DISCONTINUED EARLY IN THE TEST PROGRAM JULY 1973 BECAUSE OF CONTINUED
OPERATING PROBLEMS WITH NOZZLE FAILURE AND SUBSEQUENT PLUGGING OF THE
MARBLE BED. THIS SYSTEM BECAME OPERATIONAL IN APRIL 1973, AND IT WAS
SHUT DOWN PERMANENTLY IN JULY 1973.
                                              210

-------
                                       BACKGROUND  INFORMATION
                                                 ON
                                  SHAWNEE  NOS.  10  A,  106,  AND IOC

     IN  JUNE 1968, THE EPA INITIATED  A PROGRAM  TO  TEST PROTOTYPE WET LIME AND LIMESTONE  SCRUBBING
SYSTEMS  FOR REMOVAL OF SULFUR DIOXIDE AND  PARTICULARS FROM FLUE GAS.  THE PROGRAM rtAS CARRIED  OUT
IN A  TEST  FACILITY INCORPORATED  INTO  THE FLUE  GAS  DUCT WORK OF UNIT NO.  10,  A COAL-FIRED BOILER AT
THE TVA  SHAWNEE POWER STATION, PADUCAH,  KENTUCKY.   TVA IS  THE CONSTRUCTION AND FACILITY  OPERATOR  AND
THE BETCHEL CORP. IS THE MAJOR CONTRACTOR  AND  TtST DIRECTOR.

     THE TEST FACILITY CONSISTS  OF  THREE PARALLEL  SCRUBBER SYSTEMS OF PROTOTYPE SIZE TREATING  PART
OF THE FLUE GAS FROM THE BOILER.  EACH SCRUBBER TRAIN IS CAPABLE OF TREATING APPROXIMATELY  30,000
ACFM, OR THE EQUIVALENT OF APPROXIMATELY 10  MW  OF  POWER PLANT GENERATING CAPACITY.

     THREE PARALLEL WET SCRUBBER  SYSTEMS WERE  SELECTED FOR THE TEST PROJECT: 1) A VENTUHI WITH  A
3PRAY TOWER AFTER ABSORBER:  2) A  TURBULENT CONTACT ABSORBER (TCA AND 3)  A MARBLE-BED ABSORBER.   THE
VENTURI SYSTEM, MANUFACTURED  BY  CHEMICAL CONSTRUCTION CO., CONTAINS AN ADJUSTABLE THROAT THAT
PERMITS CONTROL AND VARIATION OF  PRESSURE  DROP  UNDER A WIDE RANGE OF FLOW CONDITIONS.  THE  TCA  UNIT,
MANUFACTURED BY UNIVERSAL  OIL PRODUCTS,  EMPLOYS A  FLUIDIZED BED OF LOW DENSITY PLASTIC SPHERES  THAT
ARE FREE TO MOVE  BETWEEN RETURNING  GRIDS.   THE  MARBLE-BED  ABSORBER, SUPPLIED BY COMBUSTION  ENGINEER-
ING CO., USES A PACKING OF 3/«-INCH GLASS  MARBLE SPHERES AND A TURBULENT LAYER OF LIQUID AND  GAS
ABOVE THE MARBLE  LAYER TO  ENHANCE MASS  TRANSFER.

      THE TEST FACILITY WAS DESIGNED SO  THAT  MODIFICATIONS  AND VARIATIONS OF  SCRUBBER INTERVALS  AND
PIPING COULD BE READILY EMPLOYED FOR EACH  SCRUBBER SYSTEM.  EACH SYSTEM CAN  TREAT APPROXIMATELY
30,000 ACFM OF FLUE GAS AT 300 F CONTAINING 1800 TO 4000 PPM OF SOa AND Z TO 5 GRAINS/SCF OF  PART-
ICULATES.   TESTING OF  THE  TCA AND THE VENTURI  SPRAY TOWER  IS IN PROGRESS: OPERATION OF THE  MARBLE-
BEO  ABSORBER UNIT HAS  BEEN PERMANENTLY  DISCONTINUED.
                                                  211

-------
                 TABLE 12
DESCRIPTION OF TERMINATED FGD SYSTEMS   01/78
UTILITY NAME          UNION ELECTRIC CO.

UNIT NAME             MEREMAC NO. 2

UNIT LOCATION         ST. LOUIS COUNTY MISSOURI

UNIT RATING            110 MW

FUEL CHARACTERISTICS  COAL   3.4 PERCENT  SULFUR

FGD VENDOR            COMBUSTION ENGINEERING

PROCESS               LIMESTONE INJECTION/WET  SCRUB

NEW OR RETROFIT       RETROFIT

START UP DATE          3/68

FGD STATUS            TERMINATED

EFFICIENCY,
  PARTICULATES         99 PERCENT


  S02                  83 PERCENT


WATER MAKE  UP         CLOSED LOOP


SLUDGE DISPOSAL


UNIT COST


OPERATIONAL           THE FIRST COMMERCIAL  SCRUBBER  APPLICATION  ON  A  UTILITY  COAL-FIRED BUILEK
  EXPERIENCE           OCCURRED AT THIS STATION  IN  EARLY  1968.  THE  SCRUBBING STRATEGY INCLUDED
                      LIMESTONE INJECTION INTO  THE FURNACE  WITH  AN  EXISTING COAL PULVERIZER AND
                      TAIL-END SCRUBBING  WITH  THE  CALCINED  REAGENT  IN TWO  MARBLE-BED ABSORBERS.
                      THIS FULL-SCALE EXPERIMENTAL SCRUBBING  PROGRAM  WAS EVENTUALLY TERMINATED
                      AND THE INSTALLATION  WAS  ABANDONED. PROBLEMS  ENCOUNTERED INCLUDED BOILER
                      TUBE FOULING BECAUSE  OF  CLOSE  TUBE  SPACING,  WIDESPREAD  SCALING,  SEVERE
                      CORROSION, INEFFICIENT MIST  ELIMINATOR  AND PROBLEMS  WITH WASTE DISPOSAL.
                                             212

-------
                             TABLE  13
              TOTAL FGD MEGAWATT CAPACITY  BY  YEAR  *
                  YEAR
NO. UNITS MEGAWATTS
1968
1971
1972
1973
1971
1975
1976
1977
1978
1979
1980
1981
1982
1983
1984
1985
1986
UNDEFINED
1
1
4
a
2
4
5
10
19
15
23
11
7
7
3
2
2
10
125
400
260
1410
250
1054
2198
«853
7718
6031
9658
5805
3353
3735
2050
1300
1100
4029
* TOTALS DISPLAYED DO NOT INCLUDE TERMINATED OR INACTIVE SYSTtMS.
                               213

-------
     APPENDIX A




FGO SYSTEMS ECONOMICS
         A-l

-------
                                  APPENDIX  A.    FGD  SYSTEM  ECONOMICS:    OPERATIONAL  SYSTEMS
COMPANY
PLANT
UNITS
TOTAL CAPACITY, MW
Arizona Public Service
Cholla Electric Generating
Station
No. 1
115


Columbus & So. Ohio Electric
Conesville Generating Station
No. 5
400



PROCESS
STATUS
START-UP DATE
Limestone
Operational
10/73


Lime
Operational
1/77



REPORTED CAPITAL
COSTS,
$ MILLION
6.555


15.27



$/KW
57.0


37.90



REPORTED OPERATING
COSTS,
$ ANNUAL



7.765 MM



MILLS/KWH
2.20


5.61



COMMENTS
1. Capital cost figure includes the venturi scrubbers (2)
for particulate control. This figure represents
total expenditures made by the utility through 1973.
2. Capital cost figure does not include limestone prep-
aration, sludge handling facilities and interest on
capital during construction.
3. Additional costs incurred by the system supplier have
not been reported.
4. The operating cost figure includes operating and main-
tenance expenditures only.
1. The capital cost figure includes direct costs only.
2. The capital cost figure includes two scrubber modules,
all ancillary equipment, sludge disposal system -site
preparation, and construction costs. Indirect! are
not included.
3. Annual operating costs are estimated at a load factor
39.5%.
4. Annual costs include capitalization, raw materials
waste disposal, maintenance, labor, and utilities.
5. All cost estimates are given in 1976 dollars.
 I
u>
                 Note:  N/A indicates figures are not available.

-------
    APPENDIX  A  (Continued).   FGD  SYSTEM ECONOMICS:  OPERATIONAL SYSTEMS
COMPANY
PLANT
UNITS
TOTAL CAPACITY, MW
Ouquesne Light
F.R. Phil lips Station
Nos. 1 to 6
410
Elrama Station
Nos. 1 to 4
510

















Indianapolis Power & Light
Petersburg Generating Station
No. 3
530







PROCESS
STATUS
START-UP DATE
Lime
Operational
7/73

Lime
Operational
10/75

















Limestone
Operational
10/77








REPORTED CAPITAL
COSTS,
$ MILLION


44.219

52.919



















32.082









$/KW


114

107



















61.891









REPORTED OPERATING
COSTS,
$ ANNUAL
14 MM



16.2 MM





























MILLS/KWH
COMMENTS
5.86 j 1. Total capital cost figures for Phillips and Elrama
j include all expenditures required to bring the
entire plants into compliance.

5.35





























2. Total capital cost figures include all process equip-
ment, engineering costs, contractor's fees and
interest on capital during construction. Excluded
are the costs of additional long term sludge disposal
facilities that may be required. However, equipment
for short term disposal is inc-luded ($2 MM). The
$/kW values are based upon the station's net generat-
ing capacities with the scrubbers in service. The
Phillips and Elrama Stations net generating capacities
are 387 and 494 MW respectively.
3. Annual operating cost figures of 6 mills/kWh is based
upon the combined operating costs for the Phillips
and Elrama stations when full SO? compliance is
achieved. This amounts to approximately $32 million
annually.
4. A weighted average replacement energy cost based on
system cost and purchased power cost for each plant of
13.69 mills/kWh is not included in the cost figures.
5. All costs are given in 1977 dollars except the re-
placement energy cost which is given in 1976 dollars.
1. Capital cost figure includes scrubbers, pumps, fan
reheat and all auxiliary equipment ($25.9 MM); sludge
stabilization, and disposal ($3.5 to $4.0 MM); and
indirect costs ($1 .616 MM).
2. The cost of the ESP's installed upstream of the
scrubber plant for particulate control ($4.083 MM)
is not included.
3. Interest during construction is not included.
4. FGD design and costs are based upon 4.5% sulfur coal,
which is the maximum allowable sulfur content for the
scrubber plant.
Note:  N/A indicates figures are not available.

-------
                APPENDIX  A   (Continued).    FGD  SYSTEM  ECONOMICS:    OPERATIONAL  SYSTEMS
COMPANY
PLANT
UNITS
TOTAL CAPACITY, MW
Kansas City Power & Light
La Cygne Power Station
No. 1
820




Kansas Power & Light
Lawrence Energy Center
Nos. 4 & 5
525



PROCESS
STATUS
START-UP DATE
Limestone
Operational
2/73




Limestone
Injection &
Wet Scrubbing
Terminated,
Operational
12/68 & 11/71



REPORTED CAPITAL
COSTS,
$ MILLION
52.4




3.5



$/KW
63.9




7



REPORTED OPERATING
COSTS,
$ ANNUAL
5.35 MM

MILLS/KWH
1.402




N/A





N/A



COMMENTS
1. The capital cost figure includes $45.4 million in
expenditures already made plus an additional $7
million required to reach optimum system performance
($5.2 million for the installation of an eighth
scrubber module) .
2. The annual operating cost figures include operating
labor and materials, maintenance labor and materials,
limestone and reheat energy.
3. The annual operating and maintenance cost figure is
based upon a 1976 capacity factor of 53%.
4. A replacement energy cost of 8.8 mills/kWh is not
included in the cost figures.
5. Cost estimates are given in 1976 dollars.
1. The capital cost figure presented represents a sum
paid by the utility for both systems in 1968. Ex-
penses incurred in many subsequent modifications
over the years were largely underwritten by the
system supplier. Therefore, the figures listed are
unreal istical ly low and are not meaningful.
2. These units have been and are now being replaced with
venturi rod scrubber and spray tower systems utiliz-
ing a limestone-based scrubbing slurry.
3. Lawrence No. 4 rod scrubber and spray tower limestone
scrubbing system was placed in service Jan. 1977. The
original injection unit has been dismantled.
4. Lawrence No. 5 rod scrubber and spray tower scrubbing
system is now being erected. The original injection
unit is still in service. Start up of the new system
scheduled for Mar. 1978
 I
LT1
              Note:  N/A indicates figures are  not available.

-------
                            APPENDIX  A   (Continued).     FGD  SYSTEM  ECONOMICS:    OPERATIONAL  SYSTEMS
               COMPANY
               PLANT
               UNITS
               TOTAL  CAPACITY, MW
PROCESS
STATUS

START-UP DATE
REPORTED  CAPITAL
    COSTS,
                   MILLION
                             $/KW
REPORTED OPERATING
      COSTS,
                                        ANNUAL
                                               MILLS/KWH
                                                                                    COMMENTS
               Kentucky  Utilities
               Green River  Power Station
               Nos.  1, 2 &  3
               64
Lime
Operational
9/75
                                                                  3.674
                                                                            57.4
                                                                                    4.419 MM
                                                                                               2.02
 I
CTi
               Louisville  Gas & Electric
               Cane Run  Power Station
               No.  4
               178
Lime
Operational
8/76
                                                                 10.4
                                                                            58.4
                      2.5    j   N/A
                                           1.  The capital  cost figure  for  this  turnkey installa-
                                              tion includes installed  cost of FGD equipment,
                                              ancillaries, and sludge  disposal-site preparation
                                              and waste transport system.

                                           2.  The operating cost figure includes  feed material and
                                              chemicals, labor and supervision, waste disposal,
                                              maintenance materials, labor and  supervision and
                                              reheat energy cost.

                                           3.  The capacity factor for  Green River 1,2 and 3 in 1976
                                              was 47.5%.

                                           4.  A replacement energy cost of 10.04  mills/kWh is not
                                              included in the cost figures.

                                           5.  Cost figures are given in 1976 dollars.
                      1.  The total installed capital  cost  includes the install-
                          ed cost of FGD equipment,  ancillaries and sludge dis-
                          posal  - site preparation and waste transport system,
                          and the carbide lime unloading docks for all three
                          FGD - equipped Cane Run units  (Nos.  4,5, and 6).  The
                          total  also includes $85,000  to reline the exhaust
                          ductwork and stack.

                      2.  The reported annual operating cost figure includes
                          all operating and maintenance charges.

                      3.  The cost figures are given in 1977 dollars.

                      4.  A replacement energy cost  of .23  mills/kWh  is not
                          included in the cost figures.
             Note:  N/A indicates  figures are not available.

-------
     APPENDIX  A   (Continued).    FGD  SYSTEM  ECONOMICS:    OPERATIONAL  SYSTEMS
COMPANY
PLANT
UNITS
TOTAL CAPACITY, MW
Louisville Gas & Electric
Paddys Run Power Station
No. 6
65












Mlnnkota Power Coop.
M.R. Young Station
No. 2
450






Montana Power Co.
Colstrip Plant
Nos. 1 & 2
720





PROCESS
STATUS

START-UP DATE
Lime
Operational
4/73













Fly Ash/Lime
REPORTED CAPITAL
COSTS,

$ MILLION
3.38















32
Operational
$/KW
52







REPORTED OPERATING
COSTS,

$ ANNUAL
















71.11

9/77
i
1





Fly Ash/Lime
Operational
10/75 & 7/76










55.27












83.74























1.185 MM








MILLS/KWH
5.6

























0.26











COMMENTS
1. The capital cost figures are based on the boiler
rating minus system power consumption. The costs
includes everything except the final waste disposal
site. This is a borrow pit supplied by the State
highway department at no cost to the utility.
2. The operating costs include feed material and chemi-
cals, labor and supervision, maintenance materials,
labor and supervision and reheat energy cost.
3. Cost of the carbide lime absorbent is confidential.
4. Costs are atypical because the unit is used for peak
loads and the scrubber is a research and development
tool for future full scale installations now opera-
tional, under construction or planned by the utility.
5. A replacement cost of .25 mills/kWh is not included
in the cost figures.
6. The cost figures are given in 1976 dollars.
1. The total installed capital cost figure represents
an estimated value for the unit's entire emission
control system.

2. An upstream ESP for primary particulate control
($12 million) is not included.
3. The capital cost figure does not include the exten-
sive sludge handling and disposal strategy proposed
for this unit (vacuum filters and building, conveyor,
by-pass equipment, trucks and front-end loaders.
1. The reported capital cost includes foundation, field
wiring, insulation, heat tracing, painting, piping
to ponds, piping between modules, field distributions
in addition to the scrubber modules, ductwork, equip-
ment supply and erection. Also included is the
interest costs, cost of fly ash ponds, fly ash slurry
transport systems and evaporation pond, and incre-
mental costs such as auxiliary boiler, F.D. fans.
start-up and auxiliary transformer.
Note:   N/A indicates  figures are not available.

-------
             APPENDIX  A
(Continued).   FGD  SYSTEM ECONOMICS:   OPERATIONAL  SYSTEMS
COMPANY
PLANT
UNITS
TOTAL CAPACITY, MW
Nevada Power Co.
Reid Gardner Station
Nos. 1 & 2
250

Northern Indiana Public Serv.
D.H. Mitchell Station
No. 11
115


PROCESS
STATUS
START-UP DATE
Sodium Carbonate
Operational
4/74

Wellman-Lord
Operational
6/77


REPORTED CAPITAL
COSTS,
$ MILLION
11

14,825


$/KW
44

129
REPORTED OPERATING
COSTS,
$ ANNUAL
1.2 MM

6.006 MM


MILLS/KWH
N/A

8.1


COMMENTS
1. The total installed capital cost figure is an
estimate that was originally provided by the
utility for expenditures completed by installation
date (1974). Included are both scrubbing systems
along with all the raw material handling and pond
equipment cost.
2. The annual operating cost figure includes $600,000
annualized for each unit.
1. The capital figure includes interest during con-
struction and overhead charges.
2. Reported operating cost figure is a total annualized
cost value that includes operation and maintenance
costs, and anti-oxidant agent costs.
3. Fixed charges are calculated for a 10-15 year plant
lifetime (26% of $41,825 MM). Assume an annual unit
load factor of 73.5*.
4. The cost figures are given in 1976 dollars.
 I
CO
         Note:  N/A indicates figures are not available.

-------
                   APPENDIX  A  (Continued).    FGD  SYSTEM  ECONOMICS:     OPERATIONAL  SYSTEMS
COMPANY
PLANT
UNITS
TOTAL CAPACITY, MW
Northern States Power
Sherburne County Generating
Plant
Nos. 1 & 2
1420



Pennsylvania Power
Bruce Mansfield Plant
Nos. 1 S, 2
1650


Philadelphia Electric
Eddyston Generating Station
Unit No. 1A
316



PROCESS
STATUS
START-UP DATE
Limestone
Operational
5/76 & 5/77



Lime
Operational
4/76 & 7/77


Magnesium Oxide
Operational
9/75



REPORTED CAPITAL
COSTS,
$ MILLION
60



249.15


28.44



S/KW
44



151


90



REPORTED OPERATING
COSTS,
$ ANNUAL MILLS/KWH
3.77 MM



28.2 MM



0.40



4.25
COMMENTS
1. The total installed capital cost figure includes
direct costs only, indirect costs are excluded.
2. The total cost figure applies to 1976/1977 installa-
tion and does not include escalation factors.
3. The annual operating cost figure is an estimate that
applies to 1977 operations at an 80% unit load factor.
Included in this figure are direct and indirect costs.
4. The $/KW figure is based upon the net generating
capacity of both units (680 MW/unit, 1360 MW total).
5. The cost of one redundant scrubber train is included
for each system.
1 . Cost figures presented are estimates provided
by the util i ty.
2. The total installed capital cost figures includes
all direct and indirect costs plus escalation factors.
3. The cost of the venturi scrubbers required for par-
j ticulate emission control are included.
1 4. All cost figures are reported in 1977 dollars.
4.7





1. The capital cost figure includes installed cost of
FGD equipment, ancillaries, sludge disposal-site
preparation and waste transport system. The
magnesium oxide regenerating facility cost is also
included. The cost of paniculate scrubbing is also
included.
2. The operating cost figure includes feed material
disposal, maintenance materials, labor and supervision
and reheat energy cost.
3. A replacement energy cost of 12.3 mills/kWh is not
included in the cost figures.
4. The cost figures are given in 1976 dollars.
 I
VO
            Note:  N/A indicates figures are not available.

-------
             APPENDIX A  (Continued)
FGD SYSTEM ECONOMICS:   OPERATIONAL SYSTEMS
COMPANY
PLANT
UNITS
TOTAL CAPACITY, MW
South Carolina Public Service
Winyah Generating Station
No. 2
380




Springfield City Utilities
Southwest Generating Station
No. 1
200

Tennessee Valley Authority
Widows Creek Steam Plant
No. 8
550




PROCESS
STATUS
START-UP DATE
Limestone
Construction
7/77




Limestone
Operational
4/77

Limestone
Operational
5/77




REPORTED CAPITAL
COSTS,
$ MILLION
6.345




15

56 . 284




S/KW
22.66




75

102.33




REPORTED OPERATING
COSTS,
$ ANNUAL





"

5.226 MM




MILLS/KWH
0.333






1.72




COMMENTS
1. Fifty percent of the boiler's flue gas is scrubbed
for SO, removal. S0? removal efficiency is 69%.
2. The total direct and indirect cost for the ESP pro-
vided for primary particulate control upstream of the
scrubbers is $1.686 MM (not included in this
table).
3. The capital cost figures include installed cost of
FGD equipment, ancillaries, sludge disposal-site prep-
aration, and waste transport system.
4. The operating cost figure includes feed material and
chemicals, labor and supervision, waste disposal,
maintenance materials, labor and supervision and
reheat energy cost.
5. A replacement energy cost of 20 mills/kWh is not
included in the cost figures.
6. The cost figures are given in 1976 dollars.
1. The capital cost figures are actual FGD system costs
given by the Utility.
2. The $5 MM particulate cleaning cost (ESP) is not
included.
3. The cost figures are given in 1977 dollars.
1. The total installed capital cost figure is an estimate
that includes all expenditures made by February 1977.
2. Included in the total installed figure are the costs
of the existing ESP and venturi scrubbers for control
of particulate emissions, plus all direct and in-
direct costs, and escalation.
3. Sludge handling and disposal facilities are not
included in the above estimate.
4. The annual operating cost figure is an estimate that
applies to operation in 1977.
5. The annual operating cost estimate includes partic-
ulate removal costs. Amortization of investment is
not included.
6. The mills/kWh figure derived from the operating ex-
penditures is the total annual cost estimates (direct
and indirect) at a unit capacity factor of 63%.
 I
(-•
o
         Note: N/A indicates figures are not available.

-------
      APPENDIX  A   (Continued).     FGD  SYSTEM  ECONOMICS:     NONOPERATIONAL   SYSTEMS
COMPANY
PLANT
UNITS
TOTAL CAPACITY, MW
Alabama Electric Coop.
Tombigbee Power Station
Nos. 2 & 3
510





Arizona Electric Power
Apache Station
Nos. 2 and 3
400
Basin Electric Power Coop.
Laramie River Station
Nos. 1 and 2
1100


Big Rivers Electric Coop
Reid Steam Station
No. 2
250


Big Rivers Electric Coop
Reid Steam Station
No. 3
240
PROCESS
STATUS
START-UP DATE
Limestone
Construction
3/78 & 3/79





Limestone
Construction
6/78 & 4/79
Limestone
Contract
Awarded
4/80 8, 10/80


Lime
Contract
Awarded
1979


Lime
Contract
Awarded
1980
REPORTED CAPITAL
COSTS,
$ MILLION
35.464





21
80


10.81


rio "
-i . -----
$/KW
69.54





5.25
68.2


43.24


i
REPORTED OPERATING
COSTS,
$ ANNUAL
240,323







MILLS/KWH
0.77






1.5











COMMENTS
1. Capital cost figures includes S02 scrubber trains,
limestone milling facilities, sludge treatment and
disposal pond, engineering costs, contractors fee
and interest on capital during construction.
2. 70% of the flue gas capacity is scrubbed.
3. Annual operating costs are calculated for 1978 with a
60% boiler capacity factor.
4. Included in the operating costs are all direct costs
minus maintenance and solid waste disposal costs.
5. Indirect costs are not included in the operating cost
figure provided.
6. A replacement energy cost of 15.5 mills/kWh per boiler
is not included in the cost figures.
1. Reported capital. cost includes the 4 scrubbers, 2 feed
tanks, recycle pumps, piping and instrumentation.
Lime handling equipment, the ESP's and waste disposal
system is not included in the figures.
1. The reported capital cost figure provided in the table
applies to the total installed cost for both double-
loop wet limestone scrubbing systems including waste
disposal, piping, and sludge handling.
2. Breakdown of the capital cost is not available.
3. Reported operational cost is an estimate as of
December 1977.
1. The reported capital cost figure applying to the
amount of the contract awarded to AAF for the turnkey
emission control installation was $16 million,
$5.19 million of which covered paniculate controls.
2. All figures are reported in 1976 dollars.
3. The $16 million figure includes an AAF-ELEX ESP, two
spray towers, reheater, ancillary equipment, ductwork,
and modular pre-wired control rooms.
1 . The contract awarded amounted to greater than $10
million for the FGD system.
 I
H-
M
                Note:  N/A indicates  figures are not available.

-------
            APPENDIX A (Continued).   FGD  SYSTEM ECONOMICS:   NONOPERATIONAL  SYSTEMS
COMPANY
PLANT
UNITS
TOTAL CAPACITY, MW
Boston Edison Company
Mystic Power Station
No. 1
155




Central Illinois Light Co.
Duck Creek Power Plant
No. 1
400




PROCESS
STATUS
START-UP DATE
Magnesium Oxide
Terminated
4/72




Limestone
Construction
8/78




REPORTED CAPITAL
COSTS,
$ MILLION
9.510




37.328




S/KW
63.4


REPORTED OPERATING
COSTS,
$ ANNUAL
615,000




93.32








MILLS/KWH
3.0




3.31



1
COMMENTS
1. All cost figures are reported for the project com-
pletion date of 1974.
2. The total installed capital cost of the Rumford cal-
cination facility was approximately $4.5 MM.
3. Capital charges are not included because of non-
applicability to a 2-year demonstration program.
4. Operating costs for the acid plant regeneration
facility are not included.
5. The cost of make-up magnesium oxide ($150/T) is not
included.
6. 3.0 mills/kWh is an estimate for total operation and
maintenance costs, including calcination.
7. BECO and EPA each subsidized approximately BOX of the
costs of the demonstration program. Chemico also
underwrote some of the program costs.
1. The capital cost figure is an estimate of system
expenditures, including the cost of the installation
of the FGD system ancillaries, the limestone milling
and waste disposal facilities.
2. One module has been completely installed and tempo-
rarily operated from September 1976 to April 1977.
Full system operation is scheduled to commence in
August 1978.
3. The annual cost includes feed material and chemicals,
labor and supervision and $3.390 million for the
sludge/ash disposal pond as well as the power con-
sumption cost.
4. The replacement energy cost of 10 mills/kWh is not
included in the cost figures.
5. Cost figures are given in 1976 dollars.
 I
M
to
          Note: N/A indicates figures are not available.

-------
                APPENDIX  A   (Continued).    FGD  SYSTEM  ECONOMICS:    NONOPERATIONAL  SYSTEMS
COMPANY
PLANT
UNITS
TOTAL CAPACITY, MW
Central Illinois Public Serv.
Newton Station
No. 1
575

Colorado Ute Electric
Craig Station
Nos. 1 & 2
900



Commonwealth Edison
Powerton Station
No. 51
425


PROCESS
STATUS
START-UP DATE
Double Alkali
Construction
11/79

Limestone
Construction
03/79



Limestone
Construction
12/79

REPORTED CAPITAL
COSTS,
$ MILLION
108.5

105



50

S/KW
189

117



117.65

L_^
REPORTED OPERATING
COSTS,
$ ANNUAL


15 MM





. - ..
MILLS/KWH


2.7



8.70


COMMENTS
1. The capital cost figure is an estimate covering all
the scrubber unit operation areas.
2. Capital figure is quite high because of the deliber-
ate overdesign and redundancy incorporated into the
system for achievement of reliable operations.
3. The $/kW figure is calculated on the unit's net
generating capacity of 575 MW. 3% of the unit's net
generating capacity is required to power the scrubber
plant.
1. The total capital cost figure is an estimate provided
by the utility that does not include reagent prepara-
tion and sludge disposal facilities.
2. The total revenues of the contract awarded to Peabody
Engineered Systems for two limestone slurry spray
tower scrubbing systems is expected to exceed $60 MM.
3. Electrostatic precipi tators are included in the
capital cost figure.
4. The annual operating cost figure is a preliminary
utility estimate based upon a 70% load factor.
1. The total installed capital cost expenditures apply
to the following timetable: all expenditures will be
made from May 1976 to December 1978; expenditures
of $16 MM will be made from October 1976 to October
1977.
2. The annual operating cost is an estimate which in-
cludes the following items:
0 2.7 mills/kWh for operation and maintenance.
° 6.0 mills/kWh for auxiliary power requirements.
0 Scrubber life span is estimated for an annual
usage rate of 148,000,000 kWh. This is equivalent
to approximately $900,000 annual for auxiliary
power consumption.
>
 I
             Note:  N/A  indicates figures are not available.

-------
            APPENDIX  A  (Continued).    FGD  SYSTEM ECONOMICS:    NONOPERATIONAL SYSTEMS
COMPANY
PLANT
UNITS
TOTAL CAPACITY, MW
Commonwealth Edison
Will County Station
No. 1
167







Detroit Edison
St. Clair
No. 6
163







Gulf Power
Scholz Steam Plant
Nos. 1 & 2
23

Gulf Power
Scholz Steam Plant
No. 2
20

PROCESS
STATUS

START-UP DATE
Limestone
Terminated
2/72


REPORTED CAPITAL
COSTS,
REPORTED OPERATING

COSTS,
i

$ MILLION
15.542










Limestone
Terminated
5/76








Dilute Acid,
Terminated
2/75


Dry Adsorption
Terminated
2/76






13.089










3.0




N/A





$/KW $ ANNUAL
113 3.985 MM















80.3







MILLS/KWH i COMMENTS
13.06 '' 1. The capital cost figure includes the venturi scrubbers
for particulate control.









9.60






i ;




130




N/A







N/A




N/A





N/A




N/A





2. The $/kW figure is based upon the unit's maximum net
generating capacity with the FGD system, 137 MW.
3. The annual operating cost figure is based on a system
lifetime of 14 years. Sludge treatment costs include
handling to an off-site disposal area. The figure
provided is the cost to own and operate the scrubbing
system for 1975.
4. Unit load capacity factor for 1975 was 49.4%.
1. The capital cost figure includes the installed FGD
cost, ancillaries, sludge disposal -site preparation,
and waste transport system.

2. The annual operating cost figure includes feed mat-
erial and chemicals, labor and supervision, waste
disposal, maintenance materials, labor and super-
vision, and the cost of reheat energy.
3. All costs are given in 1976 dollars.
4. The replacement energy cost of 9.0 mills/kWh is not
included in the cost figures.
1. The total installed capital cost figure provided for
the CT-101 prototype unit includes the scrubbers and
ancillary equipment, engineering costs and contractors
fee. This figure is not representative of a full-
scale application.
1. Actual cost figures for this prototype unit are not
available. Foster Wheeler has published initial
capital cost figures which range from $25 to $35 per
kW for low sulfur removal efficiency and $70 to $75
per kW for high sulfur removal efficiency.
>
I
        Note:  N/A indicates figures are not available.

-------
                 APPENDIX  A   (Continued).    FGD  SYSTEM  ECONOMICS:     NONOPERATIONAL  SYSTEMS
COMPANY
PLAN!
UNITS
TOTAL CAPACITY, MW
Illinois Power
Wood River Power Station
No. 4
110









Kansas City Power & Light
Hawthorn Power Station
Nos. 3 & 4
525










PROCESS
STATUS
START-UP DATE
Catalytic
Oxidation
Terminated
10/72



REPORTED CAPITAL
COSTS,
$ MILLION
8.5







i




Limestone
Injection &
Wet Scrubbing
Terminated
11/72













5.32









$/KW
82.5












19
REPORTED OPERATING
COSTS,
$ ANNUAL
952.000































MILLS/KWH













2.2-2.5






















COMMENTS
1. Reported capital cost figure represents the total
expenditures during the 2.5 year duration of the
program.

2. The $/kW figure is based upon the system's net
generating capacity of 103 MW.
3. ESP cost is included since upstream fly ash removal
is a necessary feature of this regenerable system.

4. The annual cost figure is an estimate representing
system running costs only. Excluded are capital
charges and a credit for product. This figure trans-
lates into a value of $3.46 per ton of coal consumed.
1. This figure is unrealistically low because these
installations were experimental in nature and were
heavily underwritten by the system supplier.

2. This system has been terminated as limestone-based
system and converted to a wet lime scrubbing system.
The costs of additional slakers, feeders, and other
necessary equipment are not included.
3. Sludge disposal facilities are not included in the
total cost figure.
4. The annual operating cost figure does not include
fixed costs.
5. The replacement energy cost of .058 mills/kWh is not
included in the cost figures.
 I
h-1
LT!
            Note:  N/A indicates  figures  are  not  available.

-------
            APPENDIX A  (Continued]
FGD SYSTEM ECONOMICS:   NONOPERATIONAL SYSTEMS
COMPANY
PLANT
UNITS
TOTAL CAPACITY, MW
Key West Utility
Stock Island Power Plant
37



Louisville Gas & Electric
Cane Run Power Station
No. 5
183
Louisville Gas & Electric
Cane Run Power Station
No. 6
277
Montana Power Co.
Colstrip Plant
Nos. 3 & 4
1400
Pacific Power & Light
Idaho Power Company
Jim Bridger Plant
No. 3

PROCESS
STATUS
START-UP DATE
Limestone
Terminated
10/72



Lime
Construction
12/77
Double Alkali
Construction
2/79
Fly Ash/Lime
Contract
Awarded
7/80 & 7/81
Sodium Carbonate
Construction
9/79

REPORTED CAPITAL
COSTS,
$ MILLION
0.750



12
16.3
N/A
50-60 MM

$/KW
20.7



66
58.9
N/A
110-120

REPORTED OPERATING
COSTS,
$ ANNUAL





7.3 MM
N/A


MILLS/KWH
0.7





N/A


COMMENTS
1. This system was jointly funded by the EPA and the
utility. The system supplier has also underwritten
a considerable amount of the capital expenditures.
This figure, therefore, is unreal istical ly low.
2. The utility has had to pay for the cost of a new
primary crushing system.
3. The operating cost figure provided was an original
estimate and has not been corroborated or disputed
by actual experience. This estimate was based upon
the following factors:
° Capitalization rate of 10%; no taxes, no insurance.
0 Maintenance cost of 5% of equipment cost.
° Labor cost at $20,000 per year.
0 Limestone cost at $4.05 per ton.
1. The total installed capital cost is an estimated
figure that includes the costs of lime handling and
sludge disposal facilities.
1. The total installed capital cost figure is an estimate
provided by the utility.
2. The annual operating cost figure provided is an
estimate for one year's service following the first
three months of operations. $4.5 million of this
total will be subsidized by the EPA for technology
research, development and report writing. This sub-
sidy will not be utilized for any capital expenditures
1. Capital cost figures are currently not available for
publication. The contract awarded to the system
supplier is expected to exceed $50 MM for both units.
1. The total installed capital cost figures are estimated
values provided by the utility.
2. The system will be comprised of 3 parallel absorption
towers each handling 33.3% of the flue gas capacity.
3. The reagent, a nominal 30 wt. % Na?C03 purge solution,
will be purchased from a local soda ash manufacturer.
I
h-J
CTi
         Note:  N/A indicates figures are not available.

-------
                   APPENDIX  A   (Continued).     FGD  SYSTEM  ECONOMICS:    NONOPERATIONAL   SYSTEMS
               COMPANY
               PLANT
               UNITS
               TOTAL CAPACITY, MW
PROCESS
STATUS

START-UP DATE
REPORTED CAPITAL
    COSTS,
                                                                    MILLION
                              $/KW
REPORTED OPERATING
      COSTS,
                       ANNUAL   M1LLS/KWH
                                                                                       COMMENTS
               Potomac Electric Power
               Dickerson Station
               No. 3
               190
Magnesium Oxide
Terminated
9/73
                     6.5
                               68
                     990,000
            N/A
1.   The total  installed capital  cost figure is an estimate
    provided by the utility in 1973.

2.   This figure does not include regeneration and acid
    plant costs.

3.   The operating cost figure is an estimate provided
    for 1974 operations.  This figure includes operation
    maintenance costs and acid plant freight and  opera-
    tion charges.   Not included  in  this  figure are fixed
    charges, utility charges,  project management  and
    engineering costs.
 I
I—1
-J
               Public Serv. Co.  of Colorado
               Valmont Station
               No. 5
               50
Limestone
Terminated
10/74
                                                                     4.35
                                                                               87
                                            1.  The capital costs reprsent $44/kW for the particulate
                                               scrubber installed in 1971 and $43/kW for the cost of
                                               the retrofit slurry treatment equipment installation
                                               in 1974 to control the pH of the scrubber slurry.

                                            2.  The SOj removal system was installed as a research
                                               and development project.  It was not operating long
                                               enough for the utility to determine an annual operat-
                                               ing cost.
               Public Service of New Mexico
               San Juan Station
               Nos. 1 & 2
               715
Wellman Lord
Construction
11/77
                                                                    89.510
                                                                              127.87
                                                                                       7.236 MM !    5.0
                                           1.  The total installed capital cost figure is an esti-
                                               mated value that applies to 1977 installation.   In-
                                               cluded are all direct and indirect costs plus an
                                               escalation factor.

                                           2.  The $/kW figure is based on a net generating capacity
                                               of 700 MW.

                                           3.  The costs of the venturi scrubbers for particulate
                                               removal are included in the total cost figure.

                                           4.  The cost of one redundant scrubber train is included.

                                           5.  The annual operating costs  and the mills/kWh value
                                               derived are estimated for 1978 operations  and based
                                               upon a capacity factor of 77%.

                                           6.  No credit is allowed for by-product recovery (this
                                               includes both the elemental  sulfur product  and  the
                                               sodium sulfate purge product for use in  pulp and paper
                                               processes.
                Note:   N/A  indicates figures are not available.

-------
              APPENDIX A  (Continued).    FGD  SYSTEM  ECONOMICS:   NONOPERATIONAL SYSTEMS
COMPANY
PLANT
UNITS
TOTAL CAPACITY, HW
Salt River Project
Coronado Station
Nos. 1 t, 2
700



So. Indiana Gas 4 Electric
A.B. Brown Station
No. 1
250




PROCESS
STATUS
START-UP DATE
Limestone
Contract
Awarded
4/79 & 4/80



Double Alkali
Construction
4/79




REPORTED CAPITAL
COSTS,
$ MILLION
69



10.8




S/KW
98

REPORTED OPERATING
COSTS,
$ ANNUAL




43.2










MILLS/KWH
2.8



1.08




COMMENTS
1. The contracts for the ESP and scrubbing system have
been awarded. The combined cost of these two new
power-generating facilities, including emission con-
trol is estimated at 685 MM.
2. Total capital and operating costs are estimated as
1978 dollars.
3. Total capital costs include direct material and
construction costs, engineering, contingencies,
escalation and interest during construction.
4. The operating costs include energy and demand costs,
limestone supply, operating and maintenance, and
capital carrying charges. Sludge disposal is not
included.
1. FMC was awarded a contract in excess of $8 million for
the design and installation of a double alkali
scrubbing system.
2. Total expensitures for this new plant are estimated
at $134 MM.
3. The total installed capital cost figure includes in-
stalled cost of FGD equipment, ancillaries, sludge
disposal-site preparation and the waste transport
system.
4. The operating cost figures include feed material and
chemicals, labor and supervision, waste disposal as
well as maintenance materials, labor and supervision
and reheat energy costs.
5. The replacement energy cost of 7 mills/kWh is not
included in the cost figures.
6. Costs are given in 1976 dollars.
 I
M
CO
         Note:  N/A indicates figures a^e not available.

-------
   APPENDIX  A   (Continued).     FGD  SYSTEM  ECONOMICS:    NONOPERATIONAL  SYSTEMS
COMPANY
PLANT
UNITS
TOTAL CAPACITY, MW
Southern Mississippi Power
R.D. Morrow Generating Plant
Nos. 1 & 2
360


Texas Utilities Co.
Montecello Station
No. 3
750
Wisconsin Power & Light
Columbia Plant
No. 2
527

PROCESS
STATUS
START-UP DATE
Limestone
Construction
11/77 & 6/78


Limestone
Construction
2/78
Fly Ash/Lime
Letter of
Intent
1/80

REPORTED CAPITAL
COSTS,
$ MILLION
13.447


18.5
30
i
i
$/KW
37.35


25
57

REPORTED OPERATING
COSTS,
$ ANNUAL




4.2 MM

MILLS/KWH






COMMENTS
1. The total installed capital cost figure is a 1975
estimate.
2. Included in the cost figure are the scrubbers
and ancillary equipment, fans, construction
field expenses, and interest during construction.
3. The ESP costs, ($5.4 MM equipment costs for two
units) are not included.
4. Sludge handling and disposal facilities are not
included in the total cost figure.
1. The capital cost figures include the installed cost
of FGD equipment, ancillaries, sludge disposal-site
preparation and waste transport system.
1. The total installed capital cost figure is a pre-
liminary estimate that includes the scrubbers and
ancillary equipment, erection, disposal piping and
basin area.
2. Sludge handling and disposal equipment and the up-
stream ESP are not included in this figure.
3. The operating cost figures provided are estimated
values.
Note:   N/A  indicates figures are not  available.

-------
                      APPENDIX B



               FGD PROCESS FLOW DIAGRAMS



THIS APPENDIX COMPRISES BOTH ACTIVE AND INACTIVE UNITS



     ARRANGED ALPHABETICALLY ACCORDING TO UTILITY
                        B-l

-------
ca
 i
U)

                                                                                          I    MODULE (3)


                                                                                         jAi;;:f:''
L :-:•,:•.• : '.-.-.-'r --<•;,? 1
1
«^-,.;. 1





!
i »
'J2

^y7
'








- 3









:









F

X





i:
<
X












i


t »

"

                                   Arizona  Public Service,  Choi la No.  1  FGD System:
                                                  General  Flow Diagram.

-------
03
I
                               Arizona  Public Service,  Four Corners  Prototype  Scrubber Module:

                                                  Cross Section  Diagram.

-------
            BOILER
            FLUE
            GAS
W
 I
ui
                                                                                          SULFURIC ACID
                                                                                          CONTACT ACID
                                                                                              PLANT
 98% GRADE
- H2S04
                                      MgSO-.6  HO
                                      HgSO^.7
                                      MO
      AIR
                                          PUMP
                             Boston  Edison, Mystic No. 6  FGD System  and Essex  Chemical Plant
                                      Regeneration Facility:   Schematic  Flow Diagram.

-------
                            MIST
                            ELIMINATOR
W
 I
CTl
   RILEY
VENTRI-SORBER
  SCRUBBER
                LIMESTONE
                 SLURRY
                                                                             ELECTROSTATIC
                                                                             PRECIPITATOR
                                                        SCRUBBER
                                                        I D BOOSTER FAN
t »
RECYCLE TANK

                                                                                                           RECYCLE
                                                                                                           TO FGD
                                                 PUMP                            SETTLING POND
                                                 Central  Illinois Light Co.,
                                             Duck  Creek  Mo. 1  FGD System Module:
                                                 Simplified Process Diagram.

-------
                                                                                                              CLEAN GAS
TO
 I
                 SERVICE
                 WATER
                FLUE GAS
                                                                                          I	STEAM  _   I
                                                                                        NOT NECESSARY f?'SUFFICIENT
                                                                                          REHEAT GAS IS AVAILABLE
                           LIME  SLAKING
                           AND DILUTION
 WASTE
DISPOSAL
 SYSTEM
                                Columbus  and Southern Ohio Electric, Conesville  No. 5  FGD System:
                                                         Process  Flow Diagram.

-------
Commonwealth Edison, Will County No. 1  FGD System
             General Process Diagram.

-------
w
i
         MAKE UP WATER FRESH


                    N ID FAN
           UNIT  5
           NORTH BIN
              r\
     LIMESTONE
       MIXING
       TANK
                                                                                                   SPRAY WATER
                                                                                                   SURGE TANK
                                               #6 FUEL OIL

                                              IGNITION GAS

                                              AlR~
                                            SPRAY WATER PUMP
                                                                                                 WASTE SLURRY TO
                                                                                                          »
                                                                                                 DISPOSAL POND
             FROM DISPOSAL'
             POND      CLEAR WATER
                          PUMPS
                                   WASTE SLURRY
                                   PUMPS
                                    ABSORBER
                                    RECYCLE PUMPS
LURGI RECYCLE
   PUMPS
WASTE SLURRY
SUMP
                                       Detroit  Edison, St. Clair No. 6 FGD System:
                                                General Process Diagram.

-------
w
I
                                               1ST STAGE
                                               ADJUSTABLE VENTURI
                                               FOR FLY ASH/S02
                            RECYCLE RETURN SYSTEM
                 CaS03/S04

                 FLY ASH SLURRY
                                 RETURN TO POND
'THICKENE
                             ASH POND

                             TO
                       STABILIZATION
                         FACILITIES
                                                                 2ND  STAGE
                                                                 S02  ABSORBER  SCRUBBER
                                                                              REHEATER
                                               STACK
                                              jL
LIME SILO


     I |-gLAKER
                                 SLURRY j^U-]
                                  TANK
o
i—
•=£
                                      Duquesne Light, F. R. Phillips FGD System:
                                                   General Diagram.

-------
w
 i
                         TEST  STACK
       FLUE  GAS
       BLOWER
                     PRESCRUBBER
                        L__J
          '  r~i
  THICKENER
WASTE
DISPOSAL
                                                                                        LIMESTONE
                                                                                        SILO
                                            REHEATER
                                                         NO.  2  FUEL  OIL
                                                   MIST
                                                   ELIMINATOR
                                           ABSORBER
                                                      ^
                                                                              SULFURIC
                                                                              ACID
                                                                              TANK
                                                                        AIR
                                                     OXIDIZER
                                                            CATALYST
                                                            TANK
WASTE
DISPOSAL
                                                                    MOTHER
                                                                    LIQUOR
                                                                    TANK
                                                                                                       CRYSTALLIZER
                                                                                               CENTRIFUGE
                                                                                                            GYPSUM
                                  Gulf Power,  Chiyoda Throuqhbred  101  FGD  Prototype:
                                              General Process  Diagram.

-------
                                                         SCRUBBED

                                                            GAS
Cd
 i
                                                           VACUUM WATER RECOVERY

                                                                     L.
                                                                                                     SOLIDS
                                   Gulf Power,  Scholz CEA/ADL  Dual  Alkali  Prototype:

                                              General Process  Diagram.

-------
w
 I
I—
OJ
                                                                 REGENERATION
           REDUCTION    (21
 ADSORPTION  SECTION

 1.   INLET FLUE
     GAS  DUCTING,  DILUTION AIR
     DESIGN, AND ADSORPTION
     SECTION OVERALL LAYOUT.
 2.   ADSORPTION DISCHARGE FANS.
 3.   ADSORBER DISCHARGE FEEDERS
     CONVEYORS AND SITE GLASSES
     WHICH SHOW CHAR MOVEMENT.
 4.   ADSORBER FEED CONVEYORS.
 5.   CHAR BUCKET ELEVATORS.

 REGENERATION SECTION

 6.   AIR  PREHEATER, SAND
     FLUID BED HEATER,  HOT
     SAND BUCKET ELEVATOR.
 7.   START UP AIR HEATER.
 8.   SATURATED CHAR SURGE
     TANK, SATURATED CHAR
     FEEDER,  REGENERATOR.
 9.   SA'JD HEATER BLOWER.
 10.  SAND MAKE UP HOPPER,
     FEEDER.
 11.  HOT SAND CONVEYOR.
 12.  CHAR-SAND SEPARATOR
     FEEDER.
 13.  REGENERATED CHAR
     COOLER.
 14.  REGENERATED CHAR
    BUCKET ELEVATOR, CHAR
    MAKE UP  HOPPER, FEEDER.
 REDUCTION SECTION

 15. COAL  MAKE UP HOPPER.
    FEEDER FEED BUCKET
    ELEVATOR.
 16. COAL  FEED BIN.
 17. COAL  FEED BIN ACTIVATOR,
    ROTARY COAL AIRLOCK,
    RESOX START UP HEATER.
 18.  RESOX REACTOR.
 19.  SULFUR CONDENSER, TAIL
    GAS BLOWER.
 20.  CONTROL AIR BLOWER.
21.  ASH DISCHARGE FEEDER
22.  ASH RECEIVER VESSEL,
    WEIGH SCALE.
23.  SULFUR STORAGE TANK,
    SULFUR TRANSFER PUMP.
                                         Gulf Power,  Scholz  FW-BF  Dry  Adsorption Prototype:
                                                       General  Equipment  Schematic.

-------
Cd
I
                                                                                      CAT-OX MIST
                                                                                      ELIMINATOR
              FLUE GAS
            FROM EXISTING
               ID FAN
                                                                                                        STORAGE
                          Illinois Power,  Wood River No.  4  Catalytic Oxidation  FGD System:
                                               Simplified  Process  Diagram.

-------
W
 I
M
Ul
                             COAL
                             SUPPLY
                                                           STACK
                                                                           .D. FAN.
          IIMESTONE
          SUPPLY
rEEDER
                                          AIR HEATER

                                             DEMISTER-
                       PULVERIZER
                                                                RECYCLE
                                                                PUMP
                                                                                                        CLARIFIER
                                                                                        MAKE UP
                                                                                        WATER

                                                                                    TO ASH DISPOSAL
                                                                                    POND
                                                  Kansas City  Power and Light,
                               Terminated Hawthorn  No. 3 FGD  System:  General  Process  Diagram.

-------
                          COAL
                          SUPPLY
to
 i
    LIMESTONE
    SUPPLY
          FEEDER
                                                          STACK
•STACK GAS

 AIR HEATER
    DEMISTER-
      MARBLE-
      BED
                                                                      —•n~-r^.-<*r"7:^^r^
                                                                      ^•f,, •-, ~> •-,'-•• ^ • .
                                                                      ^Wfii^v^.'r^'
                                                          STACK GAS
                                                          SCRUBBER
                                                                RECYCLE
                                                                PUMP

                                                Kansas City Power  and  Light
                                           Terminated Hawthorn No.  4 FGD Svstem:
                                                 General Process Diagram.
•STACK GAS
REHEATER
                              ,DRAIN  POTS
                                                                                                            CLARIFIER
                                                    MAKE UP
                                                    WATER

                                               TO ASH  DISPOSAL
                                               POND

-------
                                                      STACK
                                                                        D.  FAN
Cd
I
              COAL
              SUPPLY


                FEEDER
            PULVERIZER
STACK GAS
REHEATER
                                                      STACK GAS
                                                      SCRUBBER
                                                             RECYCLE
                                                             PUMP

                                Kansas  City  Power  and Light, Hawthorn Units 3 and 4:
                           Simplified Process  Flow Diagram of the Lime Scrubbing Process
                         LIME
                         PREPARATION
                         TANK
                       CLARIFIER
                     MAKE  UP
                     WATER

                TO ASH DISPOSAL
                POND

-------
03
I
t—'
oo
                                 Kansas City Power  and  Light,  La  Cygne No.  1  FGD System:
                                                     General  Diagram.

-------
                                                      STACK
w
 i
        COAL SUPPLY-
               FEEDER
            PULVERIZER
                                                                        I.D.  FAN
STACK GAS

  IR  HEATER

     DEMISTER

  MARBLE BED-
•STACK GAS REH1IATER
                                                              STACK
                                                                GAS
                                                             SCRUBBER

                                              Kansas  City  Power  and Light,
                                    Original  Operational FGD  System at  Lawrence No. 4.
                                                                                                         RECYCLE
                                                                                                         WATER

-------
                  FLUE GAS
DO
I
NJ
O
ROD SCRUBBER
                o
                00
                                                            SPRAY TOWER
                                                A
                                                 ^EFFLUENT  LINE
                           Kansas City Power and Light,  Lawrence No.  4 Operational  FGD System:
                                                Simplified Flow Diagram.

-------
                                                        STACK
                                                                         i.D. FAN
CO
 I
to
         COAL SUPPLY-
FEEDER
              PULVERIZER
STACK GAS REMITTER
                                      IR HEATER

                                         DEMISTER


                                       MARBLE BED-
                                                                STACK''
                                                                  GAS
                                                               SCRUBBER
                                              Kansas City Power and Light,
                                           Original  FGD System Installed at Lawrence Mo. 5;
                                            Simplified Process Flow Diagram.
                                                                                                           RECYCLE
                                                                                                           WATER

-------
CO
 I
t-0
NO
                                                              SPARE
                                        Kentucky Utilities,  Green River FGD System:
                                                 General  Process Diagram.

-------
W
 I
to
U)
                                                 K7
                                                          153.000 udn
                                                           V  360 F-
Cool-fig sprays '10 qr>m

 \  63 -177 cfm 101 F

  \\
                       Steam generator
                        250.000 IL/nr
                       1250 ps, 950 F

1


Roller
3 tph
I
i
— i
V,
                                                                               Product cyclone


                                                                            /  Surd* b.r,

                                                                           f   6 ton
                                                                               Gt

                                                                               CJPOCIIV
                                                                         ID li-t-dur  *

                                                                         20 
-------
                                                                        QUENCHER
W
I
                                                                                 DEMISTER
                             ELECTROSTATIC
                             PRECIPITATOR
                   BOILER
                    FLUE
                    GAS
                                                                                 CONTACTOR
                                                                                 SCRUBBER
                                                                                 - MODULE
                                                                                CONTACTOR
                                                                                 SCRUBBER
                                                                                 MODULE
                                     Louisville  Gas and  Electric, Cane Run  No. 4  FGD System:
                                                  Simplified Process  Flow Diagram.

-------
Cd
I
ro
Ul
                                                                   ,„
              I*) SA5 BtHEfl? F R
                                                                         50GPM FHPSH WATER ( AVE )
                                                                        Z5OGPUFWESH WATER {WAX. SHORT-TERM)

                                                                             pH 6 OR HIGHER
                                                  Louisville Gas and Electric,
                                                  Paddys  Run No. 6 FGD System:
                                                     Process Flow Diagram.

-------
     FLUE GAS
to
i
NJ
              PLENUM
                   BLEED
                               SPRAY
                             MIST
                             ELIMINATORS
                          RECYCLE PUMPS
                                                           EMERGENCY WATER
                                                            PLUMB  BOB
                                                                    *-CLEAN FLUE GAS
	SEAL WATER SUPPLY
UNDERSPRAY   ^MAKE-UP WATER
                                                               TRAY RECYCLE
                                                    47
                                          FLYASH POND
                                                                                                      POND RETURN
                                                                                   WASH TRAY POND
                                    Montana  Power  and  Light,  Cnl strip FGD Sys-terns:
                                                General  Process  Diagram

-------
                                             FRESH
                                             WATER
                                             INLET
                                               BACKWASH
                                               SPRAYS
                      STACK GAS
                      FROM I.D.
                      FANS
                       PARTICULATE
                       SCRUBBER
W
I
M
-J
HUMIDIFIED
GAS STREAM
                                                                              LLhAil U/\^> UU
                                      MIST ELIMINATORS
                                    MIST ENTRAPMENT SEPARATOR
                                   Mg (OH)2 SLURRY
                       PARTICULATE
                       SCRUBBER
                       SURGE  TANK
                                       VENTURI ROD MODULES
               S02 SCRUBBER
               SURGE TANK
                                     TO WASTE WATER
                                     TREATMENT SYSTEM

                                           Philadelphia Electric Co.,
                                           Eddystone No.  1  FGD System:
                                             General Process  Diagram.
                                                                                       SCRUBBING SLURRY INLET
                                                                                           TO Mg S03
                                                                                            RECOVERY

-------
w
 i
to
oo
                      FLUE GAS
                        TO
                      SCRUBBER
                                        REHEATER
                       FIRST
                       STAGE
                      000
FLUE GAS
TO STACK
  RIVER
MAKE-UP
 WATER
                                          MIST
                                        ELIMINATOR
                                       OVERFLOW POTS
                                        &  MARBLE BED
                     OXIDIZER
                                      REACTION
                                        TANK
                                                                                  WEIR
                                                                        THICKENER
       RECIRC
        TANK
THICKENER
UNDERFLOW
  PUMP
                                                      SPRAY
                                                      PUMP
                                        LIMESTONE—i
                                               SLURRY
                                                TANK
                                                                                                                        SLURRY
                                                                                                                         PUMP
                                                                                                                 ASH POND
                                                                                                               RETURN PUMP
                                             Northern  States  Power Co.  Sherburne  No.  1  and  2 FGD system
                                                            Simplified  Process Diagram.

-------
to
i
to
                                                                                                   TO RESERVOIR
                               Pennsylvania  Power  Co.,  Bruce Mansfield No.  1  FGD System:

                                               Simplified Process Diagram.

-------
                                             DISCHARGE
                                             TO STACK
                                                                                             CONDENSER
                                                                                            r^EVAPORATOR/
                                                                                                 CR'YSTALLIZER
                             PRESCRUBBER
                           (VARIABLE-THROAT
                                  VENTURI)
03
I
U)
o
FLUE GAS FROM
    UNIT #11
       FLY ASH PURGE TO POND
                                                    TRAY  TOWER
                                                     ABSORBER
                                               TREATED
                                            PURGE STREAM
                                                     SODIUM  SULFATE
                                                          CAKE
                                                                                           Qj COMPRESSOR
                                           DRIED
                                          SULFATE
                                          PRODUCT
                                            Northern Indiana Public Service,
                                    D.  H.  Mitchell  No.  11  Wellman.Lord/Allied System:
                                                General  Process Diagram.

-------
03
 I
LO
                                                                      5'F

                                                                    67.000 ACFM
                              .TA:K)
                              ^~"
DESIGN
AK3IENT
A[«|

  b^-^
 r£&^
STEAM 763T
    474 PS:A
    476.7 LB/KIN
                           BYPASS
                           DAMPER
                   473,000 ACFM
                     350'r
ISOLATION 169 -f
__ DAMPER 1 485.000 AC
T
'
i SCIATIC;!
OAWERS ^
3500 HP
FM

"1
119'F 3G4.400 AC
/
OEM!
SIEVE
                                                                                                                   ms-IT x-TEa FR:
                                                                                                                       123 VX
                           6 1?M


                        PUXP SCALS

pH 7
PC:;O


PC
«:!CV
0
                                     Nevada  Power, Reid Gardner FGD Systems,  Units 1,  2,  and  3:
                                                          General  Process  Diagram.

-------
Cd
 I
LO
tsj
FLUE GAS BY-PASS j

1ST STAGE
LECTRO-STATIC
PRECIPITATOR

r

J c
i
x\
?,wra
                    TO DRY ASH HANDLING SYSTEM
        n
X-
          ASH POND
TRANSFER -,

       S^
!       _±_
! CENTRATE  |
\   TANKl   J

        i
        i
        i
        i
                                                   —>J
                                    MgO FROM
                                   ACID PLANT
                                                                           HH SCRUBBER/ABSORBER
                                                                       AIR
                                                                 ___>JFUEL
                                                                                  MgS03 TO ACID PLANT
                                           Potamic  Electric and Power,
                                    Dickerson No. 3  Regenerative FGD  System:
                                            General  Process Diagram.

-------
w
 I
U)
u>
                              FLUE GAS TO REHEATER



                                DEMISTER WASH
                                                                                             LEASE EQUIPMENT
                                  SCRUBBER  BALLS
                                  (3)  SECTIONS
                                                                                           SOLID  WASTE DISPOSAL POND



                                                                                        MAKE-UP WATER
                                  TO SEAL WATER
                                     Public  Service  Co.  of  Colorado,  Valmont Station No.  5:
                                                  Modified Scrubber  Flow Diagram.

-------
Cfl
I
u>
   ALKALI
STORAGE SILO
                 SLURRY  9
                MIX  TANK
                                                 FLUE GAS FROM
                                                 PRECIPITATORS
                                                  CONTROL
                                                  BUILDING
          MOTOR  CONTROL
  THICKENER  CENTER
OVERFLOW TANK
                                                        ABSORBE
                                                        HOLD  TANK
 POWER
1 PLANT
 STACK
                              ALKALI
                            MIX TANKS
                                                                          TURBULENT
                                                                          CONTACT
                                                                          ABSORBER
                                       Southern  California  Edison,
                                   Mohave No.  1  Vertical  Test Module:
                                       Simplified  Process Diagram.

-------
CO
I
OJ
                                                FOUR  SCRUBBER  STAGES
                                                                                          >C
                           HOT  AIR
                          INJECTION
                  J
                  BOOSTER FAN
MIST ELIMINATOR
                         Southern  California  Edison, Mohave Mo. 2 Horizontal Test Module:
                                              Simp!ified Side View.

-------
03
 I
U>
CTi
                                       MAKEUP WATER)
                                                      I.D. FAN
                 SCRUBBER\Y
     SAMPLE POINTS

     OGAS COMPOSITION
     ®PARTICIPATE COMPOSITION & LOADING
     ©SLURRY OR SOLIDS COMPOSITION
	GAS STREAM
	LIQUOR STREAM
                                                                                               ]	
                                                                                      PROCESS
                                                                                       WATER
                                                                                       HOLD
                                                                                       TANK
                                                                                                     STACK
                                                                                               ^MAKEUP WATER[
                                                                                     DISCHARGE
                                                        SETTLING POND
                                             Tennessee Valley Authority,
                                         Shawnee No. 10 Prototype Test Unit:
                                              General Process Diagram.

-------
                                                                I.D. FAN
03
i
LO
         SAMPLE POINTS
         OGAS COMPOSITION
         ®PARTICIPATE COMPOSITION & LOADING
         ® SLURRY OR SOLIDS COMPOSITION
	GAS STREAM
	LIQUOR STREAM
                          PROCESS
                           WATER
                         HOLD TANK
                                                                                       VACUUM
                                                                                       FILTER
                                                       STACK
                                                                                                 0
                                                                                                  DISCHARGE
                                                                                                      =j
                                               SETTLING  POND
                            Tennessee  Valley  Authority, Shawnee No. 10 Prototype Unit:
                                             General Process Diagram.

-------
                              FLUE GAS
    MAKE-UP WATER
to
I
to
CO
                      SPRAY TOWER EFFLUENT
                            HOLD  TANK
                                                           OXIDATION
                                                            TANK
                                                                        VENT   AIR
                                                                         A
                                                                                CLARIFIED LIQUOR
                                                                                     WATER
                                                                                            CfcD
T
 I
           BLEED TO
         DEWATERING
            SYSTEM
                                                                                      DESUPERSATURATION
                                                                                            TANK
                         Tennessee Valley Authority, Shawnee No.  10 Prototype Test Unit:
                       Modified Venturi/Spray Tower System for 2-Stage Oxidation Testing.

-------
ca
i
OJ
                                                                               REHEATER

                                                                                   ENTRAPMENT SEPARATOR
                                                                                                          FLUE GAS DUCT
                                                                                                         FROM POWER HOUSE
                                                                                                 EXISITNG ESP'S
                                                                             FANS


                                                                          VENTURI CIRCULATION TANKS


                                                                  ABSORBER CIRCULATION TANKS
                                                       ABSORBER CIRCULATION PUMPS
                                             Tennessee Valley Authority
                                         TVA Widows Creek No. 8 FGD System:
                                                  Schematic Diaaram.

-------
CO
I
                             TO  STACK
                                        ^U I S^" I  ^U^
                                                     REHEATER
                                                      DEMISTER
                                                    RECYCLE
^-MARBLE  BED

     SPRAY
                    FLUE  GAS
                    FROM  V R
                    BOILER


                      HEAT
                    EXTRACTOR
  •LADDER

   VANES
                                                                     WATER
    LIQUID
                                 DISPOSAL
        -VACUUM   FILTER
                               Union Electric Co., Meremae No. 2 FGD System:
                                   Simplified Process Flow Diagram of
                                 Injection and Time-End Scrubbing System.
                                                                                     CLARIFIER

-------
 APPENDIX C




DEFINITIONS
     C-l

-------
                                                DEFINITIONS
   Boiler  Capacity  Factor:
   Boiler  Utilization  Parameter:
   Efficiency:
        Particulates
        SO,
o
i
LO
        FGD Viability Indexes
(kWh generation in year)/(maximum continuous
generating capacity in kW x 8760 hr/yr).

Hours boiler operated/hours in period,  expressed
as a percentage.
The actual percentage of particulates removed by
the emission control system (mechanical collectors,
ESP,  or fabric filter and FGD) from the untreated
flue gas.

The actual percentage of SO2 removed from the flue
gas by the FGD system.   Design removal efficiency
values are presented for nonoperational systems or
for operational systems for which actual removal
data are not available.

Several parameters have been developed to quantify
the viability of FGD system technology.   Various
terms such as "availability,"  "reliability,"
"operability," and "utilization"  are used to
accurately represent the operation of any FGD
system during a given period.   The above-mentioned
parameters are defined below and  discussed briefly.
The objectives of this  discussion are to make the
reader aware that several different definitions
are being used and to select appropriate parameters
that can be used for reporting purposes  so that
reasonably consistent comparisons can be made.

-------
                                                DEFINITIONS
        Availability Index
        Reliability Index
o
i
        FGD Operability Index
Hours the FGD system is available for operation
(whether operated or not)  divided by hours in
period,  expressed as a percentage.   This parameter
tends to overassess the viability of the FGD
system because it does not penalize for election
not to operate the system when it could have been
operated.  Boiler downtime may tend to increase
the magnitude of the parameter because FGD failures
generally cannot occur during such periods.

Hours the FGD system was operated divided by the
hours the FGD system was called upon to operate,
expressed as a percentage.  This parameter has
been developed in order not to penalize the FGD
system for elected outages, e.g., periods when the
FGD system could have been run but was not run
because of chemical shortages, lack of manpower,
short duration boiler operations, etc.  The main
problem in using this formula is the concise
determination whether or not the system was "called
upon to operate" during a given time period.  In
addition, an undefined value can result when the
FGD system is not called upon to operate for a
given period (e.g., turbine or boiler outage when
FGD system is available).

Hours the FGD system was operated divided by boiler
operating hours in period, expressed as a percentage
This parameter indicates the degree to which the
FGD system is actually used, relative to boiler
operating time.  The parameter does not reflect
the extent of exertion on the FGD system, that  is,
the magnitude of the parameter has little or no
correlation with FGD system operating time.  Also,
the parameter is penalized when options are exer-
cised not to use the FGD system in periods when
the system is operable.  In addition, an undefined

-------
                                                    DEFINITIONS
       FGD Utilization Index
n
FGD Status:
     Category 1

     Category 2
       Category  3
        Category  4
        Category  5
       Category  6
value can result when the FGD system  is not  called
upon to operate for a given period  (e.g.,  turbine
or boiler outage when FGD system is available).

Hours that the FGD system operated divided by
total hours in period.  This parameter is  a
relative stress factor for the FGD system.   It is
not a complete measure of FGD system viability
because the parameter can be strongly influenced
by conditions that are external to the FGD system
(e.g., infrequent boiler operation will lower the
value of the parameter although the FGD system may
be highly dependable in its particular application)

Operational - FGD system is in service removing SO-

Under Construction - ground has been broken for
installation of FGD system,  but FGD system has not
become operational.

Planned, Contract Awarded - contract has been
signed for purchase of FGD system but ground has
not been broken for installation.

Planned, Letter of Intent Signed - letter  of intent
has been signed, but legal contract for purchase
has not been awarded.

Planned, Requesting/Evaluating Bids - bid  requests
have been released but no letter of intent or
contract has been issued.

Considering only FGD Systems - an FGD system is
proposed as a means to meet an SO2 regulation.

-------
                                                     DEFINITIONS
        Category 7


        Category 8
n
i
   FGD Vendor
   Fuel Characteristics
   New
   Nonregenerable
   Operational Experience
   Process
   Regulatory Class
Considering an FGD system as well as alternative
methods.

Nonoperational - FGD system has been in service in
the past but has been shut down permanently or for
an extended indefinite period of time.

A firm which fabricates and supplies FGD
systems,  most notably the flue gas treating and
ancillary equipment.

Type of fuel, average gross heating value in
Btu/lb. average percent ash and average percent
sulfur content for fuel as fired.

FGD unit and boiler were designed at the same
time or space for addition of an FGD unit was
reserved when boiler was constructed.

The S02 removed from the flue gas is not recovered
in a usable or marketable form and resulting sulfur-
bearing waste products must be disposed in an
environmentally acceptable fashion.

Summary of FGD status and description of current
month's progress.

Company name if process is patented.  Generic name
if several companies have similar processes.

A.   New boiler constructed subject to Federal New
     Source Performance Standards.

B.   Existing boiler subject to State Standard
     that is more stringent than the Federal New
     Source Performance Standard  (NSPS).

-------
                                                 DEFINITIONS
   Regenerable
   Retrofit
   Sludge Disposal
n
i
   Start-up  Date
   Total  FGD  System Lost
   Unit  Cost
C.   Existing boiler subject to  State  Standard
     that is equal to or less stringent  than NSPS.

D.   Other  (unknown, undetermined).

The SO2 removed from the flue gas  is recovered
in a usable or marketable form  (e.g.,  sulfur,
sulfuric acid, gypsum, ammonium  sulfate, sodium
sulfate).

FGD unit must be added to an existing boiler not
specifically designed to accommodate FGD unit.

Disposal method for nonregenerable systems producing
sludge including:   lines or unlined ponds,  stabil-
ized or unstabilized sludge, and on- or off-site
disposal,  disposal type (minefill, landfill,
structural fill).   For the regenerable systems,
the form or method of sulfur recovery is provided
(e.g.  - molten elemental sulfur,  sulfuric acid
plant).

Date when initial  S02 removal began or is scheduled
to begin.

The total  monthly  lost generation hours due to FGD
train outages divided by the total monthly  expected
generation if the  FGD trains would have been
available  for operation,  expressed as a percentage.

Capital Cost in $/kW including:   SO2 absorption and
regeneration system,  SO2 recovery system, solids
disposal,  site improvements, land, roads, tracks,
substation,  engineering costs,  contractors  fee and
interest on capital during construction.

-------
                                                     DEFINITIONS

                                      Annualized Cost in mills/kWh including  fixed  and
                                      variable costs.  Fixed costs include:   interest on
                                      capital, depreciation, insurance, taxes,  and  labor
                                      costs  including overhead.  Variable costs  include:
                                      raw materials, utilities, and maintenance.

   Unit Location                      City and State listed in mailing address.

   Unit Name                          Unit identification as it appears in Electrical
                                      World  - Directory of Electrical Utilities, McGraw-
                                      Hill - Current Edition - or as indicated by utility
                                      representative for installations in planning
                                      stages.

   Unit Rating                        Operational - Maximum continuous gross  generation
                                      capacity in MW; Preoperational - maximum continuous
Q                                     design generation capacity in MW.
i
oo
   Utility Name                       Name of corporation as it appears in Electrical
                                      World  - Directory of Electrical Utilities, McGraw-
                                      Hill - Current Edition - as space permits.

   Water Make-Up                      Gallons per minute of make-up water required  per
                                      MW of  capacity.

-------
                          tf-fozw,™,yTE9HNICAL REPORT DATA
                          (flease read /nuructions on the reverse before completing)
                                                       3. RECIPIENT'S ACCESSION NO.
 EPA Utility FGD Survey:  Dec '77 - Jan '78
                                l5. REPORT DATE
                                 March 1978
                                                       6. PERFORMING ORGANIZATION CODE
                                                       |8. PERFORMING ORGANIZATION REPORT NO.
 Bernard A. Laseke, Jr.
 3. PERFORMING ORGANIZATION NAME AND ADDRESS
 PEDCo Environmental, Inc.
 11499 Chester Road
 Cincinnati, Ohio  45246
                                10. PROGRAM ELEMENT NO.
                                EHE624
                                11. CONTRACT/GRANT NO.

                                68-01-4147, Task 3
  . SPONSORING AGENCY NAME AND ADDRESS
 EPA, Office of Research and Development
 Industrial Environmental Research Laboratory
 Research Triangle Park, NC 27711
                                13. TYPE OF REPORT AND PERIOD COVERED
                                Periodic; 7-77-1/78	
                                14. SPONSORING AGENCY CODE
                                  EPA/600/13
 	|	'	
 is.SUPPLEMENTARY NOTES EpA project officers are N.Kaplan (IERL-RTP, 919/541-2556) and
 J.C.Herlihy (DSSE, 202/755-8137).
 16. ABSTRACT
           The report presents a survey of utility flue gas desulfurization (FGD)
 systems in the U.S.  It summarizes information contributed by the utility industry,
 process suppliers, regulatory agencies,  and consulting engineering firms. Systems
 are tabulated alphabetically, by development status (operational,  under construction,
 in planning stages, or terminated operations), by utility company, by process sup-
 plier, by process, by waste disposal practice, and by regulatory class. It presents
 data on system design, fuel sulfur content,  operating history, and actual perfor-
 mance. It discusses  problems and solutions associated with the boilers and FGD
 systems. Process flow diagrams and FGD system economic data are appended to
 the report.
117.
                              KEY WORDS AND DOCUMENT ANALYSIS
                 DESCRIPTORS
                                           b.lDENTIFIERS/OPEN ENDED TERMS
                                               COSATI Field/Group
 Pollution
 Flue Gases
 Desulfurization
 Electric Utilities
 Waste Disposal
 Boilers
Maintenance
Pollution Control
Stationary Sources
Utility Boilers
13B
2 IB
07A,07D

15E
13A
 3. DISTRIBUTION STATEMENT

 Unlimited
                    19. SECURITY CLASS (ThisReport)
                    Unclassified
                         21. NO. OF PAGES
                             291
                    20. SECURITY CLASS (Thispage)
                    Unclassified
                                            22. PRICE
EPA Form 2220-1 (9-73)
                   C-9

-------