EPA-bOO/2-75-072
December 1975
Environmental Protection Technology Series
            ECONOMICAL  RESIDENTIAL  PRESSURE
             SEWER  SYSTEM  WITH NO  EFFLUENT
                                 Municipal Environmental Research Laboratory
                                      Office of Research and Development
                                     U.S. Environmental Protection Agency
                                             Cincinnati, Ohio  45268

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                     RESEARCH REPORTING SERIES
Research reports of the Office of Research and Development,
U.S. Environmental Protection Agency, have been grouped into
five series.  These five broad categories were established to
facilitate further development and application of environmental
technology.  Elimination of traditional grouping was consciously
planned to foster technology transfer and a maximum interface in
related fields.  The five series are:

             1.  Environmental Health Effects Research
             2.  Environmental Protection Technology
             3.  Ecological Research
             4.  Environmental Monitoring
             5.  Socioeconomic Environmental Studies

This report has been assigned to the ENVIRONMENTAL PROTECTION
TECHNOLOGY series.  This series describes research performed to
develop and demonstrate instrumentation, equipment and methodology
to repair or prevent environmental degradation from point and non-
point sources of pollution.  This work provides the new or improved
technology required for the control and treatment of pollution
sources to meet environmental quality standards.
This document is available to the public through the National
Technical Information Service, Springfield, Virginia  22161.

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                                       EPA-600/2-75-072
                                       December 1975
ECONOMICAL RESIDENTIAL PRESSURE SEWER SYSTEM

              WITH NO EFFLUENT
                     by

             Gerald F. Hendricks
               Stephen M. Rees

                 SIECO, Inc.
          Columbus, Indiana  47201
              Grant No. S801041
               Project Officer

              James F. Kreissl
        Wastewater Research Division
 Municipal Environmental Research Laboratory
           Cincinnati, Ohio  45268
 MUNICIPAL ENVIRONMENTAL RESEARCH LABORATORY
     OFFICE OF RESEARCH AND DEVELOPMENT
    U.S. ENVIRONMENTAL PROTECTION AGENCY
           CINCINNATI, OHIO  45268

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                            DISCLAIMER
     This report has been reviewed by the Municipal Environmental
Research Laboratory, U.S. Environmental Protection Agency, and
approved for publication.  Approval does not signify that the
contents necessarily reflect the views and policies of the U.S.
Environmental Protection Agency, nor does mention of trade names
or commercial products constitute endorsement or recommendation
for use.
                                11

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                                FOREWORD
     Man and his environment must be protected from the adverse effects of
pesticides, radiation, noise, and other forms of pollution, and the unwise
management of solid waste.  Efforts to protect the environment require a
focus that recognizes the interplay between the components of our physical
environment—air, water, and land.  The Municipal Environmental Research
Laboratory contributes to this multidisciplinary focus through programs
engaged in

     •  studies on the effects of environmental contaminants on the
        biosphere, and

     •  a search for ways to prevent contamination and to recycle
        valuable resources.

     The technology described in this report represents one of the first
attempts to provide improved wastewater management for rural populations
in an economical manner while incorporating concepts of recycling valuable
nutrients to the land with concomitant elimination of additional pollutant
loads on surface water resources.
                                               Louis W. Lefke
                                               Acting Director
                                               Municipal Environmental
                                               Research Laboratory
                                    111

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                                   ABSTRACT
     An economical pressure sewer system with no polluting effluent was
designed, constructed, and monitored for effectiveness.  The elimination of
groundwater infiltration and restrictive elevation tolerances associated with
a conventional gravity sewer system enabled this type of sewer system to be
installed and to function economically.  The treatment process, aerobic and
anaerobic lagoon storage with subsequent irrigation of the effluent, yielded
no more than normal volume of runoff.

     Operational problems with the pressure system resulted from inefficient
home grinder-pump units.  These problems were greatly reduced when commercial-
ly manufactured home units became available.  The treatment process functioned
as anticipated.  Because of the new sewer system, summer homes become year
around residences and new home construction exceeded expectations.  As a
result, the initial irrigation area proved inadequate for handling the actual
flows and additional irrigation area was made available at a later date.

     This report was submitted in fulfillment of Grant No. 801041 under the
sponsorship of the Environmental Protection Agency.  Work was completed as
of December 1972.
                                      IV

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                               CONTENTS
Abstract




List of Figures




List of Tables




Acknowledgements




Sections




   I




   II




   III




   IV




   V




   VI




   VII




   VIII




   IX




   X




   XI




   XII




   XIII




   XIV




   XV
Conclusions




Recommendations




Introduction




Home Unit Production Problems




Home Unit Installation Problems




Grinder-Pump Unit Evaluations




Pressure Collection System




Vacuum Collection System




Storage and Treatment Lagoon




Lagoon Effluent Irrigation Data




Laboratory Analyses




Costs and Discussion




References




Publications




Glossary
Page




 iv




 vi




 vii




 viii









   1




   3




   4




   7




   11




   16




   29




   33



   37




   52




   54




   58




   62




   63




   64

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                                   FIGURES



No.

 1    Grandview Lake Sewage Research and
        Demonstration Project System Layout                                5


 2    Locally Manufactured Grinder-Pump Unit                               8


 3    Curb Valve and Riser Installation                                   14


 4    Environment One-Unit                                                20


 5    Hydr-o-matic Unit                                                   22


 6    Tulsa Unit                                                          25


 7    Overflow  Absorption System  Details                                  27


 8    Automatic and  Manual Air  Release  Valves                             31


 9    Vacuum  Unit                                                         35


  10  Vacuum  Pumping Station

                                                                          70
  11  Plan Layout  of Treatment  Plant                                      °


  12   Lagoon  Levee Failure                                                46


  13   Lagoon  Levee Failure  Cross  Sections                                47


  14   Lagoon  Levee Failure  Cross  Sections                                47


  15   Lagoon Levee Failure Cross  Sections                                48


  16   Lagoon Levee Failure Cross Section                                 48


  17   Lagoon Site Test Boring Logs                                       50


  18   Revised Treatment Plant Layout                                     51
                                       VI

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                                  TABLES






No.                                                                   Page




1    Summary of Maintenance Frequency                                  28




2    1972 Monthly Flow Data Summary                                    40




3    Daily Flow Data for July and August 1972                          41




4    Daily Flow Data for September 1972                                42




5    Daily Flow Data for October 1972                                  43




6    Daily Flow Data for November and December 1972                    44




7    Analytical Summary                                                55




8    Analytical Data                                                   57




9    Pressure Sewer Cost Breakdown                                     59




10   Approximate Home Unit Cost Comparison                             60
                                    VII

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                               ACKNOWLEDGEMENTS


 The  following  individuals assisted in the completion of this project.

 SIECO,  Inc. -  Consulting Engineers

 Gerald  F. Hendricks, Project Manager
 Stephen M. Rees, Assistant Project Manager
 Richard L. Sanson, Design Engineer
 John F. McCaulay, Staff Engineer
 Tony Hendricks, Laboratory Manager
 Hershel B. Sedoris, Jr., Technical Aid
 Charles Hollenback, Draftsman
 David Sharp, Field Maintenance
 Larry Smith, Field Maintenance
 Lynn Higgins,  Secretary

 Farmers Home Administration  (USDA)

 Ralph Shelburn
 Cecil Rose
 James Jackson

 Indiana State  Department of Health

 William Uhl
 Steve Kim

 Environmental  Protection Agency

 Charles Swanson
 Jim Kreissl

 Grandview Lot Owners'  Association

 John Wertz
 George Noblitt
 Robert  Lindsay
 William Luzius
 Frank Hoffman
William Kendall
Mike Bova
Tom Gerken
John Sohn
Charles Shepard
Jack Riester
William Hooker                        viii

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                                    SECTION  I

                                   CONCLUSIONS

 1.   It  is  possible  to  provide  a sewage  treatment  facility meeting a  zero-
     discharge  standard for  small  communities.

 2.   Domestic sewage nitrogen and phosphate  can  largely be converted  to
     vegetation at  a reasonable cost for small communities.

 3.   Ground raw sewage  and septic tank effluent  can  be treated  by a combined
     anaerobic  and  aerobic lagoon without objectionable odors.

 4.   Ground raw sewage  caused some additional operation and  maintenance
     problems due to the nature of the solids.

 5.   Groundwater infiltration into sewer lines is  eliminated with the use
     of the pressure system.

 6.   A pressure sewage  system can be cheaper to  install than a  conventional
     gravity system in  areas of rough topography.

 7.   Operational expenses of a  pressure  sewage system are higher than those
     associated with a  gravity  system.

 8.   The home owner should be educated in the proper operation  and  mainte-
     nance of his home  unit.

 9.   No male-threaded PVC pipe  fittings  should be  used on any home  unit
     installations.

10.   Any check  valves used in the home units should have  a gate that, when
     closed, is at  an oblique  angle from the perpendicular alignment  of
     the centerline of  the flow in the pipe in order to use the gravitational
     advantage.  A free turning valve gate that  reseats  itself  after  each
     operation  proved to be  more reliable and required less  maintenance  than
     one with a fixed gate.

11.   Mechanical seals should be used in all possible applications  of  infield
     fabrication operations  to  prevent leakage due to high groundwater
     conditions during  all or part of the year.

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12.   A fused electrical  disconnect should be located next to any external
     controls of the home unit  for use by the serviceman.  Any contractor
     installing such a system for existing residences should have a flat
     rate for each utility service damaged during installation.

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                             SECTION II

                           RECOMMENDATIONS


1.  Future pressure sewer installations should strongly consider pumping
    only septic tank effluent.

2.  A program should be instituted to determine long-term maintenance
    information on the effects of the ground paper products on pressure
    sewer lines and treatment facilities.   It is  only through such infor-
    mation that a proper cost comparison between  grinder-pump installa-
    tions and septic tank effluent pumping installations can be made.

3   The efficiency and dependability of any pressure switches installed
    to prevent excessive pressures must be established before their
    use is specified.

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                                  SECTION  III

                                 INTRODUCTION
 Grandview  Lake,  located  about  10 miles  southwest of Columbus,  Indiana, is a
 manmade  lake  with  approximately 400  acres of water surface,  and is shown in
 Figure 1.   (See  glossary for metric  conversions from  English units used
 throughout this  text).

 The  lake is located  in a rural section  of Bartholomew County that is not pro-
 ductive  farm  land.   The  soil in the  area is predominately clay and, therefore,
 provides poor drainage for  crops.  Scattered areas with exposed rock surfaces
 further  reduce the agricultural value of the land.  These characteristics
 that  tend  to  keep  land prices  low also  attract land developers.  Such was the
 case  at  Grandview  Lake,  and a  recreational and residential development was
 started.

 As the Grandview Lake area  developed during the last  twenty  years, the pollu-
 tion  problems  inherently associated with a growing population began to become
 evident  to the residents.  These problems were aggravated by the lake develop-
 er's  economic  problems.

 As the number  of residences at Grandview Lake had grown, so  had the size of
 the  lake.   Financial difficulties had hampered the completion of the lake's
 dam by the original developer.  In fact, some lot owners had built septic
 systems  on the land between their dwellings and what  they anticipated as
 being the  final lake shoreline.  However, in 1960, additional funds were
 invested in the development and the dam was completed.  When the water began
 to rise  behind the completed dam, it began to cover some of  the septic tank
 absorption fields  installed by the early residents.   Some of these installa-
 tions were abandoned for new facilities on higher ground.   Some continued to
 be used  due to the ignorance of lot owners who had acquired  property and
 were  anaware of where their septic system was located.  Still others were used
 out of indifference.

 By 1967,  residents of the lakeside community were becoming increasingly aware
 of the results of septic tank effluent  failing to be  absorbed into the soil.
Not only were  some septic systems emptying directly into the lake but the
 flows from many of the newer septic tanks were causing odorous wet spots in
the lawns  and  eventually flowing into the lake.   Algae growth was increasing
rapidly in  the fertilized lake water, small coves around the lake had a
septic odor, beaches  were becoming fouled,  and some areas of the lake had soap
suds  lining the shore.  Also,  a rural water system had been  installed
 (November 1969 thru May 1970)  around the lake,  and this was helping to attract

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LOCATION MAP
                                                       PVC PIPE (G1ZE AS SHOWN)


                                                       LAOOON CELLS
                          FIGURE 1. GRANDVIEW LAKE SEWAGE RESEARCH AND
                                   DEMONSTRATION PROJECT SYSTEM LAYOUT

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more prospective homeowners and their sewage disposal problems.

The sewage problem could not be ignored if the lake was to continue to be a
desirable center of the community life.

Individuals had attempted to solve their own sewage problems by installing
various sewage disposal systems, but it was evident that a community system
was needed.  Investigation into the feasibility of installing a conventional
gravity sewer system and treatment plant proved to be prohibitively expen-
sive ($10,000 per existing house), and this approach was abandoned.

The possibility of solving the sewage problem around the lake by installing
a pressure sewage system was first formally proposed by SIECO, Inc. in July
of 1968.

Although sewage force mains had been utilized by communities for many years,
the concept of individual pumping units located at each residence was defi-
nitely an experimental proposition.   A prior attempt in Kentucky had proven
to be a failure .   However, investigation into the Kentucky project failed
to reveal the true complexity of the proposed type of system.   The engineer
anticipated that,  by properly educating the population that would be using
the system,  many of the problems on  the Kentucky project could be avoided.
Also,  the possibility of Federal research funds helped make the project
economically feasible.

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                                 SECTION IV

                        HOME UNIT PRODUCTION PROBLEMS
Normal conditions expected when bidding a construction job did not material-
ize when the Grandview Lake project was advertised for bids.   Most contractors
originally refused to bid on the project because it was something "new and
different."  Those who did bid were unreasonably high.  Eventually, a reason-
able bid for installing the system and treatment plant was received and
accepted by the owner.  However, the heart of the pressure system, the indi-
vidual home units, was rejected by all bidders as "too complicated."

The engineer's original concept of the home unit to be used on the project
was a completely-fabricated three compartment steel tank, light enough to
be easily lifted into place by a backhoe.  In an effort to keep installation
costs down, it was anticipated that the home unit fabricator would deliver
several units at a time to the job site.  The contractor could then install
the units at his own pace without paying for a special piece of equipment for
lifting the unit into place.

However, when the fabrication of the home units was rejected by the bidder,
an alternate solution was sought to using a fabricated steel tank.  The use of
a molded plastic or a fiber-reinforced plastic (FRP) tank was eliminated due
to the excessive mold or set-up cost associated with any initial production
using those materials.  A local concrete vault manufacturer did express an
interest in casting the units out of concrete.

Being the only bidder willing to produce the unit housing at a reasonable
cost  ($125.00/unit), the vault manufacturer was awarded the contract.  He also
was awarded the assembly operation, subsequently awarded to a sub-contractor,
so that a totally "packaged" unit, as shown in Figure 2, would be  delivered
to the site.

Production problems during  casting forced the vault manufacturer to increase
the wall thickness of the unit.  This added to the weight of the casting, but
did enable the casting mold to be removed without cracking the casting.  It
also provided adequate room within interior partitions in the mold for the
concrete to be poured without having voids in the finished casting.  The cast-
ing operation still required considerably more labor than originally anticipa-
ted by the manufacturer due to  the required use of vibrators to help move the
concrete into the interior  partitions.

Several months were spent eliminating problems with the mold.  When actual
production began, the manufacturer could only produce  five units per week.
It took five months to produce  the 58 units  for the project.

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f 14  1516  1011
                                                    12
  13   5
/  ^1
                                                                           9
oo
                                                                        1. PRE-CAST CONCRETE UNIT U'x4'7"x4')
                                                                       2. LID
                                                                       3. SUMP
                                                                       4. STORAGE COMPARTMENT FOR SOLIDS
                                                                       5. STORAGE COMPARTMENT FOR LIQUIDS
                                                                       6. DRY WELL
                                                                        7. GRINDER
                                                                        8. PUMP
                                                                        9. CONTROLS PANEL
                                                                       10. PROBE WIRES CONDUIT
                                                                       I 1. CONTROLLER
                                                                       12. CONTACTOR
                                                                       13. DISCONNECT
                                                                       14. GRAVITY INFLUENT  LINE (FROM HOUSE)
                                                                       15. DROP &ATE
                                                                       16. ACCESS  OPENING
                                                                       17 ELECTRICAL SERVICE (FROM HOUSE)
                                                                       18. CHECK VALVE
                                                                       19. PUMP DISCHARGE LINE (TO MAIN)
                                                                       20. PUMP SUCTION  LINE
                                                                       21. GATE VALVE
                                                                       22. MANUAL CIRCUIT
                                                                       23. AUTOMATIC CIRCUIT
                                                                       24. GRINDER DISCHARGE
                                                                       25 GRINDER INLET
                                             FIGURE 2. LOCALLY MANUFACTURED GRIND-PUMP UNIT

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 While  the  casting  manufacturer was  having his problems, the contractor doing
 the  assembly work  was  also  experiencing problems.  Problems resulted primarily
 from attaching equipment, especially the garbage  grinder, to the concrete
 casting.   The unit developed  leaks  between the wet well and the dry well.
 These  problems were eliminated by having threaded anchor plates cast into
 the  concrete.   A quick-setting hydraulic cement was used to secure all pipes
 where  they passed  through the walls of the casting.

 A  considerable amount  of time was lost due to logistic problems in obtaining
 parts.  Plastic pipe had been specified by the engineer because of its low
 cost,  corrosion-resistance  and ease of installation.  The contractor found
 that local material supply  houses did not carry the specified thickness of
 plastic pipe and had problems getting both the pipe and the required fittings.
 After  each unit was completed, the  fabricator tested it under the engineer's
 supervision.   In these tests a problem was discovered during the grinding
 cycle  of the operation.  The garbage grinder was  using twice the amperage
 indicated  by the manufacturer.  Correspondence with the manufacturer failed
 to produce a satisfactory explanation.  By closely monitoring the water level
 above  the  grinder's cutting blades  and the amperage being used, it was
 discovered that a  liquid head over  8.25 inches above the cutting blades
 resulted in  the excessive amperage.  The unit was actually pumping the liquid
 in addition  to grinding.

 The  normal operation of a garbage grinder consists of water and garbage being
 poured into  the grinding chamber without building up a significant head.
 This accounted for the  manufacturer being unaware of the situation.  When
 conditions are such in  a household  garbage grinder installation, the duration
 of excessive  power drain is usually short enough that the thermal overload
 on the grinder is  not  activated.   Any such overloading that results in the
 thermal overload stopping the grinder would probably be blamed on "something
 stuck  in the  grinder."

 The problem,  overloading due to the height of the liquid level above the
 grinder, was  solved by  adjusting the liquid level controls in the unit so that
 the head did  not exceed 8.25 inches above the cutter blades.  However, this
 meant the  storage  capacity  in the unit was reduced, thus requiring more
 operating  cycles during the usage period.

 In the event  of a  pump  malfunction, it was possible for the electrical liquid-
 level control  conduit to become submerged.   It was therefore necessary to seal
 the wires  inside of the conduit.   Waterproof putty,  aquarium sealer,  and  a
petroleum base  mastic cement proved ineffective in stopping the water.   Even-
 tually, a quick-setting hydraulic cement was used to solve the problem.

 Piping within  the  units was done with Class SDR 21 PVC pipe.  An immediate
discovery was  that  no male-threaded PVC fittings could be used regardless of
the wall thickness  (Class 120 is the minimum acceptable by the engineer in
other instances).   Metal nipples screwed into threaded female  PVC fittings
with a solvent-weld  female connection to the piping was the only type of
threaded connection  that did not break under stress  during the operation  of
the pumps.

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In one instance, a section of pipe connected to the discharge of a positive-
displacement pump withstood an estimated pressure of 105 psi and the con-
comitant increase in temperature due to a closed gate valve.  Although the
pipe expanded to almost twice its original diameter, neither the fitting,
pipe, nor weld broke.  The pump failed, however.

Schedule 40 PVC pipe was used in the units after it was discovered that
maintenance personnel and curious home owners used the pipes to stand on when
climbing in and out of the unit.
                                     10

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                                  SECTION V

                       HOME UNIT INSTALLATION PROBLEMS


Increasing the thickness of the walls and partitions strengthened the unit,
enabled mounting brackets to be cast in the wall, and made the unit too heavy
to be picked up with a backhoe.  The contractor installing the units then
arranged for the vault manufacturer to set the units into place with his boom
truck.  This tended to limit the flexibility of the home owner, engineer, and
contractor in selecting the unit location.  Alternate solutions considered
included using a large boom crane to lift the units over the houses from the
county road; flying the units into the lots with a large helicopter from
Louisville, Kentucky; using a barge equipped with a crane and placing the
units from the lake; and using a crawler-type front end loader.  The first
three alternates were eliminated due to the weight of the unit, cost, and
increased contractor liabilit}   The last was eliminated by the county commis-
sioners refusing to let any crawler equipped equipment onto the shoulder or
surface of the county road.

Faced with having to reduce the weight of the unit, the contractor decided to
set the top on the unit in the field.  Mortar, concrete, hydraulic cement,
tar, and epoxy cement were all used and proved unsatisfactory for field
installations.  The problem was solved by using RAM-NEC, a bituminous gasket
material (manufactured by K. T. Snyder Company, Houston, Texas).  In fact,
a unit could be shifted by lifting rings in the top once the top was sealed
with the RAM-NEC.  A problem arose because of this virtue—if the interior
partitions of the unit were not covered completely at their connecting point
with the top, then voids would be left between the wet and dry sides of the
unit.  The top could not be removed so the crack had to be cleaned and then
sealed with epoxy cement.  This greatly increased the labor cost of installing
the unit.

It is recommended that any field work involved creating a waterproof seal be
eliminated if at all possible.  If not, then a mechanical seal is recommended.

The home grinder-pump units were installed and connected to the piping between
the house and the septic tank of the existing houses around the lake.  Many
of the houses and their septic systems had been constructed prior to the
additional extra fill placed over the septic tank.  This meant that many of
the grinder-pump units had to be installed from 5 to 9 feet below the existing
ground surface.

The access into the compartments in the unit was then through a concrete pipe
placed over the openings.  The concrete pipe proved to be just as difficult


                                      11

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to seal as was the unit itself.   RAM-NEC proved to be the only product  that
was reasonably reliable in assuring a watertight seal.

Due to the limited flexibility in the adjustment to grade of the height of the
riser pipe over the compartment openings, the unit fabricator cast some 6-inch
tall pipe extensions for use in height adjustments of 6 to 18 inches.   These
proved to be a good idea in the office, but a failure in the field.   The rings
were 4 inches thick to prevent breakage during the field installation.   When
installed, these rings were never sealed completely.   While not having  any
openings directly into the unit's compartments, a space was left between the
sealant and the outer edge of the riser ring.  Water would collect in this
void and, upon freezing and thawing, break the seal between the rings.   The
only prevention was to apply a sand-mix coating around the outside of the
joint.  This proved to be expensive in both labor and time lost in completing
the installation.

The problems involved with leakage, broken service lines, vandalism, and
exposure to liability can be directly related to the amount of time that elap-
ses between the digging of the hole for the home unit and the backfilling of
such.  Units left overnight without being backfilled proved, time after time,
to cost the contractor lost time and money the next day.  Eventually, the
contractor refused to start installing a unit unless he could finish it
(excluding the electrical installation) on the same day.

The electrical connection of the unit was contracted independently by each
home owner.  This was done due to the uncertainty of predicting the cost of
such installations.  The location of the electrical controls was left to the
discretion of the home owner, and, therefore, no uniform location resulted.
Locations chosen ranged from outside the house under the roof overhang to
inside a linen closet in the master bedroom.  The best location, from the
service man's standpoint, proved to be the garage.  Two notable exceptions to
this were when the location chosen in the garage was above the family's food
freezer and when the home owner had a habit of locking the family's canine
member in the garage without warning the service man.

In summary, the location should be such that access to the controls is avail-
able without entering the home and without having to climb over articles stored
in front of the controls.  NOTE:  A fused electrical disconnect should be
located next to the controls for use by the service man.

It was originally anticipated by the engineer that the majority of the existing
utilities at each home could be located, to some degree, by the home owner.
This would have enabled the contractor to avoid cutting most of those services
by locating the pressure sewer service line elsewhere.  Nothing could have been
further from the truth.  With very few exceptions, the home owner's information
proved to be of no value to the contractor.

One home owner, absolutely positive of the  location of all of his utilities,
located the path for the trencher to follow.  Consequently, the contractor
followed that route and cut the water  line, the telephone  line, the electrical
line to the man's boat house, the electrical  line to a light by his driveway,
and his gas line three times.  This was the record for services cut.  The


                                       12

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average number of services cut per house was 1.3.
It is suggested that any contractor installing such a system be given a flat
amount for each service repair required when the service line is installed
according to the home owner's instructions.

A curb cock valve (See Figure 3) was installed in all of the service lines
between the system main and the home unit.  PVC valves produced by Water and
Gas Products of Tulsa, Oklahoma, were used in these installations.  These
valves developed leaks around a metal ring used to hold the gate in the body
of the valve.  When informed of this problem, the manufacturer modified his
valve and solved the problem.

An extension of 4-inch pipe was placed over each valve to enable a valve key
to be used to open and close the valve without having to dig it up.  The
extension was then capped to prevent the dirt and water from collecting over
the valve.  Two types of caps were used:

    1.  A solvent-weld one-piece cap pressed over the end of the
        pipe without solvent

    2.  A threaded plastic sewer clean out

The second solution proved to be the best because the cap remained  functional,
even when people stepped on  it.  The first type would become wedged  on  the
pipe under similar circumstances and was difficult to remove.

Several service lines were broken when cars ran over the extension  above  the
curb cock valve.  A solution to this problem would be a collapsible valve
extension, as shown in Figure 3.

Several types of service line material were used on the project.   The  following
is a summary of the various  materials used and an evalution of each:
    Type

    PVC-SDR  21
     (20-ft.  lengths)

    PVC-SDR  13.5
     (20-ft lengths)

    PVC-SDR  21
     (20-ft lengths)

    Polypropylene
      (roll)

    Polybutylene
      (roll)
Nominal
Size(inch)
 1.5
Flexibility

 Limited


 Limited


 Limited


 Good


 Good
Type of
Fittings

Solvent Weld
 Coupling

Solvent Weld
 Coupling

Solvent Weld
 Coupling

Cold-Flared
 w/brass

Cold-Flared
 w/brass
                                       13

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                              PVC  THREADED  SEWER CLEAN-OUT
                             SOLVENT WELD
                          •—4" PVC  PIPE CLASS SDR2I I.D. 4.072"
                              /'PVC PIPE CLASS  SDR 26 O.D. 4.000'
                                              TO HOME UNIT
                                 CURB VALVE
                 I "SERVICE  LINE
                              J
                                  BRICKS / STONES/CONCRETE PAD
 TAPPING SADDLE
•W/ CURB VALVE FOR
 PRESSURE TAP
  FIGURE 3. CURB VALVE AND RISER INSTALLATION
                          14

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 PVC-SDR 21   -   This was  the  easiest pipe  to obtain because it is a
 standard stock  item of most  local plumbing supply firms.  There were
 several instances where  service  lines of  this material broke due
 to  settling  of  the home  unit.  We would not encourage its use.

 PVC-SDR 13.5 - This  is not a standard item stocked by
 most  local plumbing supply firms.  However, the  0.097-inch
 wall  thickness  compared  to the SDR-21 pipe  (0.063-inch) is
 worth the difference in  price (approximately 5^/foot).
 There were no breaks or  leaks in any service lines due to
 unit  settling,  stone bruises, etc., when this pipe was installed.
 This was the best service line material used in the opinion of
 the service men.

PVC-SDR 21 (1.5  inch)   -  Satisfactory performance.

Polypropylene  -  This pipe with cold-flared brass  fittings was
relatively easy  to work with, but care had to be taken not to
bend the pipe excessively.   The  pipe would not break,  as  would
 the PVC pipe, but it would develop a kink which would restrict
 flow and eventually rupture under pressure.   Although it  costs
more than the PVC, no time is wasted waiting for a solvent to
 set up.  This is a good  service line material if the installation
 is proper.

 Polybutylene  -   Same conclusions as for polypropylene
                                      15

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                                 SECTION VI

                        GRINDER-PUMP UNIT EVALUATIONS

The Original Unit

The locally fabricated home grinder-pump unit did not prove to be effective
in grinding and pumping the domestic waste for the following reasons:

    1.  Leakage between the wetwell and drywell
    2.  Electrical control failures
    3.  The placement of the grinder
    4.  When the pressure in the main line exceeded the
        maximum head of the centrifugal pumps then the
        pumps overheated causing leaks in the plastic
        piping in the units

The largest single factor in the failure of the locally manufactured grinder-
pump unit was due to leakage problems.  Both external and internal leakage
into the drywell caused repeated electrical failures.  Although various
methods were used to solve the leakage problem, the pre-cast concrete container
was both too heavy and too difficult to make water tight to be considered
in future installations.

Electrical control failures were the second most frequent cause of unit
malfunctions.  Several problems with the electrical equipment resulted from the
electrical panel being located in the unit.  The panel was located there to
enable servicing of the electrical equipment with maximum efficiency by
allowing easy observation of equipment performance relative to electrical
adjustments.  However, in any installation of electrical equipment in a dry-
well below grade, provisions for humidity control should be considered regard-
less of size.  Funds available did not permit this on the Grandview project
and therefore the electrical panel had to be removed from the drywell.  This
resulted in additional service time during maintenance.

It had been assumed that a relatively dry compartment would be available
within which to mount the panel.  Watertight enclosures for the electrical
equipment were utilized, but condensation within the equipment enclosures
caused contactor malfunctions.    A small light bulb was installed in the
contactor housing, and this alleviated the moisture problem in the contactor.

It was anticipated that all of the equipment within the unit would be provided
with fused protection.  While being sound in theory, the idea proved to be un-
workable in the field application.  A single fused disconnect proved to be the
best arrangement for providing electrical overload protection.
                                      16

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The electrical contactor was sized based upon the manufacturer's recommenda-
tion relative to the anticipated amperage used during the operation of the
pump and grinder.  As discussed previously,  the garbage grinder used twice
the amperage expected by the manufacturer when the liquid head exceeded
8.25 inches above the cutting blades.   This  caused the total amperage to
exceed the rated capacity of the contactor.   This in turn, caused the con-
tactor to fail.  Additionally, the frequency of grinder and pump operation
was increased when the storage above the grinder was reduced.   The sturdier
construction of the next larger size contactor proved to be well worth the
additional cost.  This was an instance when deliberate over-design by the
engineer would have been beneficial in the operation and durability of the
product.

Several of the contactors that failed structurally were returned to the
supplier and forwarded to the manufacturer.   It was interesting to note that
the following year's model of contactor had been strengthened at the points
of failure observed by the maintenance crew.

Electrical probes and float switches were used in the unit and both proved
to be relatively trouble-free.  The effectiveness of the probes was somewhat
less than that of the float switches.   This could be attributed to the solids
accumulating on the probe surface.  While solids accumulated on the float
switches, it was not a problem.  The probes initially were submerged and after
the unit had been emptied were not in contact with any liquid.  This enabled
the solids to dry and form a crust which was relatively resistant to elec-
trical conductivity.  The float switch used to shut off some units remained
in contact with the liquid so that the solids did not dry and accumulation
was minimal.  It is suggested that a pressure switch or float switch is
superior to a probe control for use in a home unit.

In summary, the electrical design of any home grinder-pump unit should be as
simple as possible and capable of operating under the worst possible conditions.
Design sizing should include at least a 50% safety factor in estimating anti-
cipated amperage loads.

The locally produced grinder-pump unit was designed to store the raw waste
from the home until 120 gallons (later reduced to 80 gallons due to problems
associated with maintaining a liquid head above the grinder) had been collected.
At that time, the grinder and pump started simultaneously.

The problem with this system was that every solid object  that was put in the
home drainage fixtures had to eventually pass through the grinder.  Regardless
of the degree of customer education in the proper use of  the grinder-pump unit,
objects got into the unit that could not be ground.  This caused the grinder
to jam and either blow a fuse or activate the thermal overload protection
protector.  This meant that the home unit would then overflow into the  standby
leaching bed until the unit was repaired.

It is not realistic to provide for grinding the total solids accumulation  from
the home; therefore, some provision for removing heavy objects prior to the
grinding step should be provided.  It is interesting to note that  the Environ-
ment/One, Hydr-o-matic, and the Tulsa units all use the suction  lift of their
                                       17

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pumps to pass the sewage through their grinders, i.e., the grinder is suspen-
ded above the bottom of the sump.   This enables a heavy object such as a nail
to remain on the bottom of the sump and avoid entering the grinder.  This is
a definite asset for all three units.

Leaks developed in the piping of several of the locally manufactured units
rather consistently.  It was discovered that this was caused indirectly by
the pressure in the main line of the collection system.  When the pressure
exceeded 35 psi, the non-flushing centrifugal pumps (shutoff head  of 35  psi)
would continue to run without pumping any liquid.  When this condition per-
sisted for a significant period of time, a considerable amount of heat was
generated and caused the plastic pipe to be weakened where it was connected
to the pump.  The point of leakage was always in the threaded connection which
joined the metal and plastic pipes.  This problem was eliminated by the
maintenance of a low pressure in the main line.

While the overall performance of the locally manufactured grinder-pump units
was unsatisfactory, it is interesting to note that one unit worked successfully
for 10 months prior to replacement with no malfunction.  However, the physical
dimensions of the unit (4 ft. x 4 ft. x 4.5 ft.), its weight and the grinder
location were not suitable for general application.

Flushing Units

The original system was designed with two flushing units on each main line.
Each of these units consisted of a 1,000-gallon storage tank connected to a
pumping unit that was activated every 24 hours by a timer.  The two units'
timers on each line were synchronized to allow simultaneous pumping.  A mini-
mum flushing velocity of 3.01 feet per second was anticipated in the 3-inch
main lines.

The pump used was a Flint and Walling (Model 101) two-stage centrifugal pump
which operated very well.  While the pump was started by a timer, it was turned
off by a float valve.  Some difficulties in adjustment were experienced with
the timers utilized on the unit.  Power interruptions caused difficulties
with the timers by altering the operating period of the units.  A backup system
of power for the timer, such as a wound spring, would have been beneficial.
This feature was used when a replacement timer was required.

The flushing units were the most successful of the locally manufactured units.
These units were designed with higher available heads than other units which
permitted their operation during periods of restricted flow, due to air locks
in the main line.  However, they pumped when the normal system flow was lowest
and subsequently the line pressure was low.

The problems discussed earlier which plagued the locally manufactured units
were also found to a lesser degree on these units.  Water leakage into the
unit was reduced because RAM-NEK sealant was used, and piping leaks were re-
duced because Schedule 80 PVC pipe was used.

Actual flushing flows did not meet the Engineer's expectations.  The anticipa-
ted daily flows from the homes having flushing units were not as great as


                                       18

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expected.   One resident having a flushing unit did not occupy his home during
much of the winter, despite a past history of occupancy during this season.

A better solution would have been for the flow from several homes to have
been collected in a common storage tank for flushing liquid.

A total system of units utilizing the large storage capability and the time-
controlled pump offers countless possibilities of regulating flow rates within
a system.   An extension to the original system was installed, and the Engineer
recommended such units be installed at each house connected to the extended
line.  Their flow was to be stored and pumped at night when other flows were
reduced.

The Environment/One Unit

 The Environment/One  Unit  was  marketed in a way that was very attractive  to
 the lot owners'  at Grandview  Lake.   The  manufacturer  offered to  furnish  and
 install the residential pumping units.   Later,  a service  agreement was
 offered by the manufacturer through  its  contractor-representative.   This
 idea of a total  package program available to the owner, where no operating
 utility maintenance  program existed,  was superior to  contracting each unit
 individually.  The convenience of dealing with one supplier-installer-service-
 man far outweighed any potential cost savings to be realized through separate
 contract  negotiation by  each  o.mer.   An  Environment/One Unit, as installed,
 is shown  in Figure 4.

 The E-l Unit,  Model  210,  is a 1 horsepower motor-driven progressing-cavity
 pump with a cutting  blade attached to the suction end of  the pump's rotor.
 The progressive  cavity pump is manufactured  by the Moyno  Pump Division of the
 Robbins and Myers Company,  located in Springfield, Ohio.   Similar pumps were
 used in the 20 locally manufactured units and proved  to be very reliable.

 The Moyno pump is designed so that the metal pump rotor turns within a rubber
 stator creating  a progressive compression action.  Although there is some
 safety factor available  due to slippage between the rotor and the stator
 during periods of restricted pump discharge, for all  practical purposes, the
 pump should be considered a positive displacement type.

 If during the operation of progressing cavity pumps an abrasive particle can
 become imbedded in the stator and score the  rotor, this may eventually lead
 to failure of the stator itself.  The E-l Unit was equipped with a modified
 stator designed to reduce failures due to abrasive scoring.  However, by
 increasing the durability of the stator, the amount of slippage between the
 stator and the standard size rotor is reduced.  This  intensifies the positive
 displacement characteristic of the pump and results in the need for a thermal
 overload switch as an integral part of the unit.

 In several instances where the pump discharge was restricted completely, the
 rotor failed.  The point of failure appeared to be within the area of contact
 between the rotor and the stator.  Abrasive particles scored the surface
 of the rotor in every instance observed.  The abrasive action of the foreign
                                       19

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HEIGHT VARIES
AS NEEDED
     PRESSURE SENSING TUBE
                                                 24" DIAMETER
                                                CONCRETE PIPE W/LID
liT^f-^
smsSir GROUND LEVEL



       BREATHER

        aOVERFLOW
           INDICATOR
           (IN HOUSE)


         GATE VALVE


         UNION

    WATERPROOF SEALANT

        4" OVERFLOW
        (OPTIONAL)

         NDTOR

   1 1/4" DISCHARGE LINE

       CHECK  VALVE

     PUMP -  PROGRESSIVE
     CAVITY  TYPE

     FIBERGLASS TANK

  GRINDER
           FIGURE 4. ENVIRONMENT/ ONE UNIT (Courtesy
                    of Environment/ One)
                                20

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particle was evidently intensified by expansion of the stator due to increa5;
temperature.

The unit uses a thermal overload on the pump motor to limit the exposure to
high operating temperatures.  However, experience did not indicate that  the
thermal overload reacted quickly enough in all instances to prevent damage
to the stator.  There were several instances where unit failure was attributed
to prolonged continual pump operation resulting in the main bearing seizing
and locking up the pump.  In these instances, the overload switch failed to
operate in time to prevent damage to the unit.

During the project, an anti-siphon feature was added to the unit by the
manufacturer.  This eliminated the maintenance required due to air-locking
that was experienced on the original Environment/One Units.

The unit housing is light weight fiberglas tank with a steel plate on top.
One person could easily install one of these tanks on the construction site.
However, the grinder-pump itself weighs 140 pounds.  The units were normally
installed 30 to 36 inches below grade, and this, coupled with the pump weight,
necessitated more than one person to install or remove the pump for maintenance
purposes.  An alternative would have been to provide a single maintenance man
with a mechanical lifting device to remove the unit.

The unit is designed for installation in the basement of the house served.
Customer preference, lack of suitable space in existing homes, and access
needed for maintenance purposes resulted in outdoor installation of most of the
units.  Access to the unit below grade was made by placing a pre-cast concrete
tile over the unit and sealing it to the unit with a petroleum base sealer.
Mechanical equipment was needed to lift the concerte tile into place and the
sealant was applied carefully to prevent water leaks into the unit.

Each unit is equipped with a warning light that may be  located in the house.
This light indicates unit malfunction and is provided as a convenience for
the home owner.

The unit electrical controls were located near or  in the home electrical panel.

The Hydr-o-Matic Unit

The Hydr-o-matic units utilized at Grandview  Lake  were used under two situa-
tions - grinding and pumping raw sewage, and pumping septic tank effluent.
The grinder-pump units were less successful than those pumping only septic
tank effluent, but both types of installation required maintenance.  The
unit was very rugged, but had operational problems.  Figure 5 is a schematic
diagram of the major elements of a Hydro-o-matic grinder-pump installation.

The basic grinder-pump unit was a 1.5 horsepower submersible centrifugal pump
with grinder blades preceding the pump.  The  tank  housing was made of steel
and the unit piping was galvanized.  The grinder-pump discharge piping was
connected to the plastic service line by a hydraulically sealed discharge
flange.  Backflow  from the  system main during pump removal was prevented by
a  gate valve,  located within the tank, whose  valve stem was extended to


                                       21

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                               CONTROL
                                 BOX

                              TROUBLE LIGHT
                              RESET
                             TO POWER CORD
                          TO CONTROL CORD
                POWER  SOURCE
                  RUN  LIGHT
                / (WHITE)

                -HAND-OFF-
                AUTO  SWITCH

                TO JUNCTION
WATERPROOF
  CABLE
   SPLICE
SEAL-TITE PROTECTORS WITH
QUICK-DISCONNECT PLUG AND
RECEPTACLE

LIFTING CHAIN

1/4" THICK STEEL TANK

3/4" GALVANIZED
GUIDE RAILS

GATE VALVE


DISCHARGE PIPE

HYDRAULICALLY SEALED
DISCHARGE FLANGE

BALL CHECK  VALVE

4"  OVERFLOW (OPTIONAL)
                              SEALED MERCURY FLOAT SWITCH

                              GRINDER-PUMP
       FIGURE 5. HYDR-0-MATIC UNIT (Courtesy of
               Hydr-0-Matic)
                            22

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within inches of the top of the unit housing.   The positioning of the  grinder-
pump in the unit was controlled by guide rails on opposite sides.   A sealed
mercury float switch was used to control the grinder-pump operation.   Back-
flow into the unit from the system main was prevented between normal operating
cycles by a ball check valve between the grinder-pump and the hydraulically
sealed discharge flange.

After the gate valve was closed, the grinder-pump was removed by pulling on  a
chain attached to it.  Although the guide rails aided in removing and  install-
ing the grinder-pump, removal by a single maintenance man was still difficult
due to the weight of the grinder-pump and attached piping (approximately 85
pounds).

The location of the unit's check valve created the biggest problem with the
unit.  During periods of excessive main line pressure, the hydraulically
sealed discharge flange leaked badly.  This caused the unit to operate continu-
ously.  If the check valve had been located between the discharge flange and
the gate valve, this could have been prevented.  Several instances of check
valve failure and leakage due to fouling with solids and stringy matter also
occurred.  The ball check valve was not as satisfactory as the swing check
type.

One pump had a problem with air locking. This caused continual operation with
no liquid movement and subsequent overheating and pump failure.  The pumps
were not equipped with an anti-siphon device.  This was prevented in the
problem unit by drilling a 0.125-inch hole in the discharge pipe between the
pump and the ball check valve.

The pump control, a sealed mercury float switch, proved to require a lot of
maintenance.  The construction of the float was faulty in that it leaked.
The manufacturer has since corrected this problem.  Since the float was
installed to operate between the grinder-pump and the tank wall, one unit,
installed in smaller (20-inch) diameter tanks, malfunctioned due to a build-up
of grease and solids on the tank wall.  This crust built up until it prevented
operation of the float  switch.  The manufacturer's representative suggested
that the home owner hose down the inside of this unit periodically  to prevent
such a build-up.

Installation of the unit was restricted because there was no provision  for
extending the height of the unit  housing beyond that  specified prior  to
fabrication.  This was  a major  problem  to  the  contractor  installing the  unit.
Care should be taken in specifying  the  tank dimensions and type  to  allow for
depth variations upon  installation.

The unit controls,, excluding the mercury float switch,  were  housed outside
the  unit, usually  in the  customer's  house.  A red trouble light  came  on
during periods  of  pump  malfunction  and  a white one during normal  operation.
A  reset  button  was  provided  for use  when the  unit had stopped due to  a
temporary condition  such  as  overheating of the pump motor.   When the  reset
button would not  start  the pump,  the maintenance  people  were notified.
                                       23

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The Tulsa Unit

The Tulsa unit was a lightweight submersible grinder-pump housed in an FRP
tank with an adjustable access riser.  Plastic products were used whenever
possible in the unit.

The grinder-pump consisted of a 1 horsepower motor, housed in a stainless
steel outer casing, with a grinder-pump attached.  An installed Tulsa unit
is shown in Figure 6.

The motor proved to be dependable but slightly undersized.  The grinder-pump
was not dependable.  The grinder blades were held in place on the shaft by a
metal key.  The pump's vibrations during operation caused the key to fall out
and the shaft to spin without turning the blades.  Subsequently, the manu-
facturer welded the blades to the shaft, but this made replacement very
difficult.

The stainless steel outer casing acted as the unit's on-off switch.  An ad-
justment for regulating the duration of operation of the pump was located in
the handle on top of the motor.  Vibrations during operation loosened the ad-
justment screw.  This caused the grinder pump to run continuously or not at
all.

The unit's centrifugal pump was rated at 12 gallons per minute at 35 psi.
Actual experience indicated that performance was considerably below the
rating.

The Tulsa unit provided the largest total storage capacity of all the com-
mercial units (71 gallons).  A concrete anti-flotation collar was also re-
quired for this unit, as shown in Figure 6.

PVC piping was used in the unit.  A PVC "quick-connector" compression-type
fitting was used to connect the discharge piping from the grinder-pump to the
service line.  A PVC corporation valve was used to prevent backflow from the
system main line into the unit when the compression fitting was removed.  A
bronze check valve was used.

Initial problems were experienced with the discharge piping due to the lo-
cation of the check valve.  Originally, the check valve was located in the
vertical discharge line close to the grinder-pump.  This created two problems.
First, the grinder-pump had to be removed to service the check valve.
Second, the ground solids, particularly paper, collected on top of the valve
gate, preventing it from seating properly.  While the first problem was an
inconvenience to the maintenance men, the second meant that backflow from the
system forced the unit to cycle continually.

The check valve problems were nearly eliminated when the check valve was
moved to a short horizontal section of piping (See Figure 6) accessible to
the maintenance man without removing the grinder-pump.
                                     24

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GROUND
LEVEL "

             LOCK
             CHECK
             VALVE
       48"
 1"
           PVC
           CORPORATION
           COCK
   PVC
DISCHARGE
LINE
       30"
        I
   CHAIN  FOR
   LIFTING
   GRINDER-PUMP
                         	J    /
          MACERATING
            BLADES
                                         ADDITIONAL RISER
                                         EXTENSION AS NEEDED

                                            POWER SOURCE -
                                            SYSTEM MONITOR &
                                            CIRCUIT  BREAKER
                                            LOCATED  IN THE HOME
                                            DISCONNECT
                                            PVC  COMPRESSION
                                             COUPLING
                                                CONCRETE
                                                ANTI-FLOTATION
                                                COLLAR
                                               FIBERGLASS TANK
                                                   OVER-FLOW
                                            ELECTRICAL CORD
                                          PUMP  HANDLE AND
                                          CONTROL ADJUSTMENT
                                          SCREW


                                            SUBMERSIBLE MOTOR
                                            W/STAINLESS STEEL
                                            OUTER HOUSING
                                           SUBMERSIBLE PUMP
                      FIGURE 6. TULSA UNIT
                              25

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The Tulsa unit did incorporate some very good features.  The grinder-pump was
light enough for one person to remove easily.  The fiberglas tank was easy to
install.  The access riser was easily adjustable to different heights during
construction.  Also, when the grinder-pump operated, it did not incur a build-
up of grease and solids around the sides of the tank as did the other units.

The unit was also equipped with a remote warning light and reset button.

Additional research and development is needed to bring the unit's reliability
into an accepted range for an operating utility.  Subsequent correspondence
with the manufacturer indicates that such research is being initiated in a
project at Wichita Falls, Texas.  Results of this work are scheduled to be-
come available in the near future.

Miscellaneous

An overflow adsorption system was recommended by the Engineer (See Figure
7) for all of the home units.  However, considerable infiltration into these
systems with overflowing into home units caused increased unit operation and
increased flow at the treatment plant.

A summary of maintenance frequency by cause and type of unit is shown in
Table 1.
                                      26

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                                        13'»B MO'
NJ
                                                               ERVICE  LINE
       SEPTIC  TANK
                                                                 ROAD
                                                            FORCE MAIN
                                            -ABSORPTION  BED
                       Typical Profile of a New Residence Installation
        PRE-CAST CONCRETE PIPE

          OVERFLOW  LEVEL

                                                    -EARTH FILL
                                                    POLYETHYLENE
                                                    F:LM
                                                        PERFORATED
                                                        PVC PIPE
SEPTIC

HOME  PUMPING UNIT-O'™
                                x 'Absorption Pit Detail X-Section
                                JDR  -  (7°  SLOPE  UP)
                                                  PEA GRAVEL
                                                  ABSORPTION
                                                  BED
                                   Plan View
      NOTE: SEPTIC TANKS ARE NOT INSTALLED  WITH HOME UNITS THAT GRIND
            AND PUMP RAW SEWAGE


                               FIGURE 7. OVERFLOW ABSORPTION SYSTEM DETAILS
DESIGN CONSIDERATIONS

1 .  THE ABSORPTION PIT SHOULD
   BE AT LEAST 31 x 4'

2.  PEA GRAVEL SHOULD BE USED
   IN THE ABSORPTION BED

3.  THE ABSORPTION BED SHOULD
   HAVE A MINIMUM VOLUME OF
   500 CUBIC FEET

4.  THE LOWER ELEVATION OF
   THE ABSORPTION BED MUST
   BE ABOVE THE LAKE OR
   OTHER PONDED WATER

5.  THE ABSORPTION BED CAN
   NOT BE LOCATED WITHIN
       OF ANY WELL
                                                                      6. STANDARD RECOMMENDATIONS
                                                                         OF THE STATE BOARD OF
                                                                         HEALTH ON SEEPAGE PITS
                                                                         MUST BE OBSERVED

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                   Table 1.  SUMMARY OF MAINTENANCE FREQUENCY
                                (2-year period)
Locally
Manufactured
Cause Unit
1.
2.
3.
4.
5.
6.
7.
8.
9.
10.

Pump Failure
Grinder Failure
Piping Failure (within tank)
Electrical Failure
(excluding controls)
Control Failure
Piping Failure (outside tank)
Infiltration/inflow of water
Collection System Malfunction
Improper Installation
Miscellaneous
Totals
Maximum Number of Units
52
25
41
66
23
11
56
7
9
81
371
27
E-l
Unita
4
0
4
3
0
2
1
1
2
0
17
15
Hydr-o
-matic
Unita
8
1
7
2
10
8
0
2
2
12
52
28
Tulsa
Unit
2
2
1
0
2
0
0
4
0
5
16
2
Maintenance of the E-l units was done primarily by the manufacturer's repre-
 sentative.   The hydr-o-matic units were serviced by the manufacturer's field
 personnel as malfunctions were reported to the factory.   Therefore,  the
 figures listed above were based on the field notes taken by the engineer's
 maintenance crew and may not include all of the service calls by others.
                                      28

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                                 SECTION VII

                         PRESSURE COLLECTION  SYSTEM

The sewage collection system at Grandview Lake consisted of 28,312 feet of
3- and 3.5-inch PVC pipe installed 36 to 42 inches below the ground surface.
One main line on each side of the lake was installed to serve approximately
one half of the total inhabited shoreline.  The two lines both discharged
into a 5-inch line which terminated at the treatment plant.

Pressure from the individual home units was sufficient to pump liquid and
ground solids to the treatment plant without the use of mainline pumping
stations.  There were several problems associated with the collection system,
but the practicality of the design concept of such a collection system was
demonstrated sufficiently to encourage similar future projects.

It was the original contention of the engineer that main line check valves
were not needed because the system would be under continual pressure and such
valves would be an added installation and maintenance expense to the utility.
For economy of installation additional gate valves were not installed at
regular intervals on each line.

While the use of main line check valves should be minimized, their use
at intersections of large mains  (10-inches in diameter or  larger) and at
specific points of potential hydraulic problems should be  considered during
design.  Gate valves should be provided on lateral main  lines and at inter-
vals sufficient to isolate twenty to thirty individual customers  for any
maintenance required.

Service  line connections to the  main line while the system was  in operation
necessitated several maintenance calls.  There were leaks  due to  improper use
of the tapping tool.  However, once having experienced the results of an
improper service tap, the installer took  care  in  future  installations so that
no leaks occurred.

Additional  leaks or breaks  in  the main  line occurred  three times  due to heavy
equipment  damage,  several times  due to  earthslides, once due to improper
installation,  and  once  due  to  theft of  a  twelve  foot  section of pipe at the
end  of one  of  the  main  lines.

During the  above mentioned  line  breaks,  the  maintenance  personnel checked
the  broken  main  line  for residual  solids  accumulation.   During the initial
startup  period,  solids  accumulated sufficiently to prevent flow in one of the
two  main lines.  However,  as  the flow increased due to additional service
connections and  flushing units were  installed, the problem was solved.
                                      29

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This confirmed the engineer's contention that some provision for flushing the
main lines is vital especially in the early stages of such a system.   On four
occasions a gasoline-powered pump was utilized to flush the main lines with
lake water.

While solids accumulation presented some problems, air locking of the main
lines was the major difficulty.  The original system utilized automatic and
manual air-release valves (See Figure 8).   Eventually, additional manual
valves were installed with the recommendation that they be converted to auto-
matic ones when funds were available.  It should be noted that during normal
operation the venting of the accumulated air and sewage gas produced a minor
odor problem.

Maintenance of the automatic air release valves was not easy because a
pressurized water source was not available at each valve for backflushing.
Several instances of valves failing to open due to solids accumulation on the
mechanical linkage arm occurred.  Generally, the air release valves were a
minor maintenance problem.

One section of the main line was plagued with breaks due to the soil shifting.
Breakage due to this earth movement was later prevented by installing a
looped section of flexible pipe instead of PVC.  Interestingly enough, this
loop seemed to solve the problem.

The pipe used on the main line was specified by the engineer to be a brown
color.   This was done to enable a person installing a service connection to
identify it.  This was especially important since the area was served by a
rural water system installed before the sewer system that also used PVC
pipe.  Since the water pipe was a white color, the engineer felt that the
brown pipe would be easy to distinguish.

The possibility of requiring such pipe to be color coded and labeled "Sewer
Line" might be worth considering on future projects.  Although this could
hamper material procurement by the contractor, it should prevent accidental
cross connection between sewer and water lines.

All PVC piping was specified to conform to U. S. Department of Commerce
Standard CS 256-63 for PVC 1220 SDR 26 with 160 psi working pressure at
2000 psi tensile strength and a minimum wall thickness of 0.097 inches.
Couplings and fittings of the deep-socket type were required.  Backfilling
of pipe with a temperature of more than 65°F was prohibited.  Testing at
150 percent of normal operating pressure (but not less than 100 psi) for at
least 30 minutes was required before completion of backfilling.  After this
test and backfill completion, the pipe was required to remain full of water
under pressure.  At the end of that time a leakage test was performed.  The
150-psi leakage test required not more than 100 gallons per day per inch
of diameter for 12-foot pipe lengths or 75 gallons per day per inch of
diameter for 16-foot lengths of leakage.
                                      30

-------
AIR RELEASE
PORT

MECHANICAL
LINKAGE

    FLOAT
                     AUTOMATIC TYPE
                          38 1/2"-
                          35 1/2"-
                          34 1/4"
 C.I.  COVER
    GATE  VALVE

      CONCRETE  PIPE


  FLUSHING HOSE
            GATE VALVE
i;APCO" 400   VALVE
             BRICK
    GATE  VALVE
         CRUSHED STONE
MANUAL TYPE
    24"-
    12"
                                          FORCE  MAIN
                                                                        CURB  COCK/TAPPING SADDLE
                                         5
                       FIGURE 8. MANUAL AND AUTOMATIC AIR RELEASE VALVES

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Installation of the pressure sewer system was accomplished with two types of
trenchers, a backhoe and a small bulldozer with a small crew of manual
laborers.  When installing home units, similar needs existed with the
addition of a front-end loader and, when concrete units were involved, a
boom-truck.
                                    32

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                                SECTION VIII

                         VACUUM COLLECTION SYSTEM

Vacuum collection, another approach to the sewage collection problem,  was
attempted on a much smaller scale than the pressurized system.   In this
system, a central pumping unit maintained a vacuum in the main  line and
connected service lines.   As the home unit filled with sewage,  a valve
connecting the unit to the vacuum line opened and the sewage was drawn into
the line by the pressure differential in the line versus the atmospheric
pressure.  The sewage was then to be drawn into the central station and  pumped
under pressure into the pressurized main line of the rest of the system.

The primary advantage of a vacuum collection system was that smaller quanti-
ties of toilet flushing water would be required than with a conventional flush
toilet.  The engineer wanted to see if an adaptation of the vacuum collection
system could offer a possible alternate solution to individual grinder-pump
units by utilizing one central vacuum pump to serve several houses.

Studies by others had indicated success in moving liquids by creating
"pockets" in the transmission lines for the liquid being moved to accumulate
into "plugs."  As liquid was drawn from one pocket point to the next, the
tendency of the plug is to dissipate and the pressure to equalize.  The
increased installation cost of  installing pockets in the collection lines was
rejected.  Instead, the collection lines were designed to remain  filled with
liquid at all times.

Operation of the vacuum system  was not  successful.  The units failed  to
empty properly.   Investigation  into the reasons  for the failure did not reveal
a  specific problem.  Possible causes investigated included piping leaks,
valve  failure, incomplete priming  of collection  lines prior  to  start-up and
line obstructions, but no satisfactory  reason was discovered.

Additional problems of water  leakage into the central vacuum unit caused
repeated maintenance, and eventually the home units were  replaced by  pressure
pumping units and the vacuum  station was  abandoned.   Insufficient funds pro-
hibited  further  investment  in this area.

Specific problems or observations  peculiar to the vacuum system were:
                                       33

-------
     1.  Initial starting of the vacuum system requires careful priming
         of the collection lines.
     2.  Installation of a vacuum system would require greater care
         than a corresponding pressure system.
     3.  Leaks in the piping are difficult to locate compared to a
         pressure leak.

The vacuum central station and the vacuum home units are shown in Figures
9 and 10.
                                   34

-------
    INFLUENT LINE
    (FROM HOUSE)
GRINDER COMPARTMENT
GRINDER
OPENING
(SEALED)
DISCHARGE TO
CENTRAL VACUUM
STATION
        LID
 6" RISER
 (AS NEEDED)
 GATE VALVE
 PRECAST
 CONCRETE
 CONTAINER
      SHEAR GATE
      (REMOVED)
                                                    OVERFLOW

                                                  DRY  COMPARTMENT
  SOLENOID VALVE
                                                      WATERPROOF
                                                      SEALANT
         STORAGE
         COMPARTMENT
         LOW WATER
         CUT-OFF
         SWITCH

         SUCTION  PIPE
                     FIGURE 9. VACUUM UNIT
                                35

-------
                        DISCHARGE TO FORCE  MAIN
CHECK VALVE
NOTE:  ELECTRICAL
PANEL  MOUNTED
ON POWER POLE
                                          CHECK VALVE
                                      5'  PRE-CAST CONCRETE
                                      CONTAINER - BASE,
                                      WALLS, AND TOP
                                      ASSEMBLED IN FIELD
                                          1/4" AIR RELEASE
                                          PIPE W/FLOAT
                                          CONTROL
                                         WATERPROOF
                                         TWO CHAMBER
                                         'PRIMER TANK

                                         PLUG COCK

                                         •FLOW SWITCH
                                         .CENTRIFUGAL
                                         PUMP

                                          WATERPROOF
                                          SEALANT
         FIGURE 10. VACUUM PUMPING STATION
                          36

-------
                                 SECTION IX

                        STORAGE AND TREATMENT LAGOON
Facilities for measuring, treating and disposing of the sewage flow from the
homes connected to the Grandview Lake Sewage System consisted of a parshall
flume with a punched-tape level recorder, a storage and pumping unit,  a two-
celled lagoon, and an effluent irrigation system, and are shown in Figure 11.
Modular approach to the plant construction was utilized by the engineer in an
attempt to minimize construction costs.  Operation of the plant was to consist
of measuring the influent flow, storage of the sewage, irrigation of the
lagoon effluent, and discharge of runoff from the irrigation area of not more
than an amount equal to the natural runoff from rainfall during the irri-
gation period.

The degree of success of the treatment facilities was encouraging but fail-
ures in the physical facilities constructed created interruptions and curtail-
ment of the effective study of the treatment process.

The parshall flume with a punched-tape level recorder was the first piece of
equipment through which the flow passed in the treatment facilities.  The
parshall flume liner was fabricated by a local metal fabrication company and
precast into a concrete rectangular channel and provided with a plywood cover.
This greatly reduced the cost anticipated on such a structure, and several
contractors indicated an interest in using such an installation on other
projects.  Field installation was limited to setting the unit in place,
connecting the required piping, constructing the level recorder pit, and
installing the recorder.  There were two problems that affected the successful
operation of the level recorder.  There was rapid accumulation of ground up
paper particles on the liner and the flume did not drain properly to prevent
the buildup of liquid in the flume.  The daily flow data were collected during
a period when daily cleaning of the liner was performed by the SIECO mainte-
nance men to solve drainage problems.  A source of flushing water would have
made maintenance of the unit easier.  Any attempt to measure ground sewage
flows must take into account this paper accumulation problem.

After passing through the parshall flume, the sewage was stored in a
1,000-galIon storage tank connected to a pumping unit.  The pumping utilized
a low head high-capacity Flint and Walling centrifugal pump controlled by
probes in the storage tank.  A sampling valve was provided so that a com-
posite sampler could draw a sample representative of the total flow entering
the plant in a 24-hour period.  Paper particles fouled the control probes
and sampling valve repeatedly and groundwater infiltration could not be
completely eliminated.
                                      37

-------
O-J
00
            VALVE
            NO. 1

             PUMPING
             UNIT NO. 1
                       MAIN  LINE  FROM SYSTEM
                             PARSHALL  FLUME
                             (HEAD  RECORDER)
       SURGE TANK

       BYPASS NO. 2
                       RETURN LINE
                       ^•»

                   "VALVE

                LVALVE NO.4

              'PUMPING UNIT NO. 2

    'VALVE NO.2
'VALVE  NO.3
RUNOFF COLLECTION TANK

         DISCHARGE  TO  STREAM

   PUMPING UN IT NO. 4

            /RETURN  NO.2
              0/ALVE  NO.7

                  ^
                  VALVE  NO.6
                                                                    IRRIGATED
                                                                    HAY  FIELD
               PUMPING
               UNIT NO. 3
                                                                                  RUNOFF
                                                                                  COLLECTION
                                                                                  TANK
                                 FIGURE 11. PLAN LAYOUT OF TREATMENT PLANT

-------
A gravity overflow line was provided so that the storage tank  and pumping
unit could be bypassed.  It was designed to be used only when  the flow
entering the plant exceeded the capacity of the pumping unit.   This  unit
failed to work on three occasions.   The first time there was an air  lock in
the pipe which was remedied by providing an air relief pipe that discharged
back into the channel behind the recording device on the parshall flume.  The
second time a piece of heavy equipment had driven over the line and  caused a
break.  The third time a dead rabbit was found in the opening to the line.
It was never determined how the rabbit got into the system.

The pumping unit No. 1 and the bypass line were connected to a common line
that discharged into the bottom of the primary cell of the lagoon.  This
pipe operated well for about 10 months but then became clogged with an
unknown object or solids.  Attempts to free the pipe failed, and a new pipe
was installed.

The lagoon was a two-celled storage facility.  The primary cell, the cell
receiving the system flow, was designed as  a  facultative pond, combining
anaerobic and aerobic  biological activity.  The raw sewage flow was to be
introduced into the lower  (anaerobic)  level of the lagoon.  Short-circuiting
of the  lagoon was minimized by use of  a tee on the influent line.  The upper
 (aerobic) level of the primary cell was to  be utilized  for  irrigation into
the hay crop  and for sealing off any odor  from the anaerobic section.   The
second  cell was to be  used for irrigation  storage and polishing.

Flows anticipated at the plant were computed  as  follows:

      22 year-around homes  @ 50,000/yr  = 1,100,000 gallons

      36 weekend homes  @  50,000/yr  x  1/3 =  600,000 gallons

      Estimated annual  flow =  1,700,000 gallons  or 5.2  acre feet

Actual  flow  figures  collected  in 1972,  shown in Tables  2 through 6,  indicated
 a flow  of about  60,000 gallons per home per year.

 The primary  cell  was  designed  for  a total  volume of 1,070,000 gallons.
 Surface aerators  were  recommended  at  a future date as  needed  to maintain the
 upper zone  of the primary cell  in  an  aerobic condition.   The  secondary  cell
 was  designed for a  storage capacity of 995,000 gallons.   The  two cells
 therefore had a  total  capacity of  more than 2 million gallons.   Space was
 reserved at  the  site for another  1-acre lagoon for future needs.

 Initial filling  of  the primary lagoon was anticipated to take approximately
 one  year under ideal conditions.   However, due to the construction  schedule
 of the  facility,  waste was discharged into the lagoon in November 1970.   Since
 initial flow was limited,  due to  slow installation of the home units, the
 anaerobic section and a portion of the aerobic section of the primary cell of
 the  lagoon was filled with 102,000 gallons of lake water pumped into the
 system.   This was done to prevent  damage  to the lagoon piping during freezing
 and thawing of the  lagoon surface.
                                       39

-------
                                                TABLE 2

                                    1972 MONTHLY FLOW DATA SUMMARY
Month
July
August
September
October
November
Total
Flow
CD
540,330
429,629
501,840
451,732
501,150
Average
Flow
(GPM)
12.1
9.6
11.6
10.1
11.6
Average
Flushing
Peak Flow
(GPM)
20.9
25.0
19.3
20.8
30.7
Highest
Normal
Peak Flow
(GPM)
108.0
100.0
73.0
96.0
258.0
Number
of Active
Home Units
92
92
92
92
93
Average
(GPD)
189.5
150.2
182.0
158.1
179.6
Flow per Unit
(GPM)
.132
.105
.126
.109
.125
NOTE:  DURING NOVEMBER 1972, ON SIX OCCASIONS THE NORMAL PEAK FLOW EXCEEDED 100 GPM.  DAILY
       INVESTIGATION BY FIELD PERSONNEL CONFIRMED PROPER OPERATION OF THE RECORDING EQUIPMENT
       AND NO BUILDUP IN THE PARSHALL FLUME DUE TO LINE OBSTRUCTIONS.  FOR SUCH A FLOW THE
       PRESSURE IN THE MAIN LINE WOULD EXCEED THE SHUT OFF HEAD OF THE CENTRIFUGAL PUMPS USED
       ON THE PROJECT.  THIS WAS ATTRIBUTED TO THE SIMULTANEOUS OPERATION OF THE POSITIVE
       DISPLACEMENT E-l AND MOYNO TYPE PUMPS.
       (1) Adjusted for any days when recorder was not in operation.

-------
         TABLE 3
     DAILY FLOW DATA
FOR JULY AND AUGUST,  1972


Date
7-15
7-16
7-17
7-18
7-19
7-20
7-21
7-22
7-23
7-24
8-05
8-06
8-07
8-08
8-09
8-10
8-11
8-12
8-13
8-14
8-15
8-16
8-17
8-18
8-19
8-20
8-21
8-22
8-23
8-24
8-25
8-26
8-27
8-28
8-29
8-30
8-31
Total
Flow
(GPP)
15,000
12,400
23,200
15,700
18,400
14,400
14,400
23,200
18,800
18,800
13,100
14,100
12,500
12,500
12,400
11,200
11,500
16,600
13,700
12,700
13,700
14,000
20,200
12,400
14,800
13,100
14,800
15,800
13,000
13,500
14,800
15,000
18,800
13,800
12,000
12,400
11,800
Average
Flow
(GPM)
10.4
8.6
16.1
10.9
12.8
10.0
10.0
16.1
13.0
13.0
9.1
9.8
8.7
8.7
8.6
7.8
8.0
11.5
9.5
8.8
9.5
9.7
14.0
8.6
10.3
9.1
10.3
11.0
9.0
9.4
10.3
10.4
10.3
9.6
8.3
8.6
8.2
Flushing
Peak Flow
(GPM)
17.0
24.0
29.0
33.0
23.0
17.0
15.0
17.0
13.0
21.0
17.0
24.0
23.0
24.0
17.0
21.0
29.0
26.0
21.0
19.0
45.0
31.0
31.0
40.0
37.0
38.0
17.0
36.0
24.0
17.0
23.0
13.0
21.0
21.0
21.0
17.0
21.0
Normal
Peak Flow
(GPM)
50.0
85.0
39.0
70.0
39.0
85.0
50.0
108.0
68.0
77.0
35.0
39.0
61.0
39.0
28.0
31.0
31.0
54.0
35.0
42.0
31.0
77.0
35.0
68.0
77.0
35.0
42.0
100.0
42.0
39.0
50.0
68.0
68.0
50.0
39.0
35.0
50.0
            41

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                                TABLE 4
                           DAILY FLOW DATA
                         FOR SEPTEMBER,  1972
Date

9-01
9-02
9-03
9-04
9-05
9-06
9-07
9-08
9-09
9-10
9-11
9-15
9-16
9-17
9-18
9-19
9-20
9-21
9-22
9-23
9-24
9-25
9-26
9-27
9-28
9-29
9-30
 Total
 Flow
 (GPP)

12,400
15,400
16,400
18,400
13,700
12,200
13,100
13,100
15,400
16,400
23,200
13,100
13,000
16,000
14,800
11,800
13,100
17,700
25,500
24,400
20,200
21,300
20,200
18,600
20,000
16,600
15,700
Average
Flow
(GPM)
8.6
10.7
11.4
12.8
9.5
8.5
9.1
9.1
10.7
11.4
16.1
9.1
9.0
11.1
10.3
8.4
9.4
12.3
17.7
16.9
14.0
14.8
14.0
12.9
13.9
11.5
10.9
Flushing
Peak Flow
fGPMl
15.0
21.0
17.0
24.0
31.0
17.0
21.0
19.0
24.0
17.0
17.0
15.0
13.0
24.0
13.0
7.0
13.0
15.0
19.0
26.0
29.0
19.0
19.0
17.0
40.0
13.0
15.0
Normal
Peak Flow
fGPMl
26.0
31.0
26.0
37.0
29.0
26.0
55.0
37.0
37.0
43.0
37.0
31.0
26.0
31.0
26.0
24.0
31.0
37.0
55.0
73.0
43.0
49.0
66.0
55.0
37.0
43.0
40.0
                                42

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      TABLE 5

 DAILY FLOW DATA
FOR OCTOBER,  1972


Date
10-01
10-02
10-03
10-04
10-05
10-15
10-16
10-17
10-18
10-19
10-20
10-21
10-22
10-23
10-24
10-25
10-26
10-27
10-28
10-29
10-30
10-31
Total
Flow
CGPDI
18,400
18,600
18,400
17,900
16,400
12,700
15,400
13,200
12,500
12,400
12,400
12,100
11,800
15,000
13,500
13,500
14,400
14,000
12,800
13,800
16,000
15,000
Average
Flow
CGPM)
^\JJ. !•*/
12.8
12.9
12.8
12.4
11.4
80
. o
10.7
90
. £
o 7
o • /
8.6
8f.
• o
8 A
. T-
8 2
O • in
10.4
Q 4
«J • "
9.4
10.0
Q 7
y . /
Q Q
g!&
11.1
10.4
Flushing
Peak Flow
fGPM)
39.0
35.0
35.0
24.0
18.0
30.0
25.0
25.0
25.0
35.0
20.0
20.0
32.0
25.0
23.0
16.0
20.0
17.0
20.0
27.0
20.0
30.0
Normal
Peak Flow
(GPM)
68.0
77.0
54.0
68.0
61.0
41.0
41.0
44.0
38.4
41.0
44.0
44.0
35.0
50.9
50.9
30.0
35.0
58.0
35.0
41.0
93.3
96.0
       43

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                              TABLE 6
                          DAILY FLOW DATA
                  FOR NOVEMBER AND DECEMBER,  1972


Date
11-01
11-02
11-03
11-04
11-15
11-16
11-17
11-18
11-19
11-20
11-21
11-22
11-23
11-24
11-25
11-26
11-27
11-28
11-29
11-30
Total
Flow
(GPP)
14,300
17,100
13,700
12,400
12,200
15,000
15,400
30,000
27,900
17,300
14,700
16,000
15,100
18,400
19,900
16,100
15,400
16,400
10,100
16,700
                              Average
                               Flow
                               (GPM)
                              Flushing
                              Peak Flow
                                (GPM)
9.9
11.9
9.5
8.6
8.5
10.4
10.7
20.8
19.4
12.0
10.2
11.1
10.5
12.8
13.8
11.2
10.7
11.4
7.0
11.6
29.0
31.0
44.0
23.0
21.0
26.0
34.0
26.0
76.0
29.0
29.0
29.0
19.0
26.0
34.0
31.0
26.0
31.0
26.0
24.0
                            Normal
                           Peak Flow
                             (GPM)

                            101.0
                             80.0
                             47.0
                             41.0
                             55.0
                             59.0
                             84.0
                            108.0
                            257.0
                            134.0
                             49.0
                             52.0
                             43.0
                             49.0
                             73.0
                             62.0
                             62.0
                             37.0
                             76.0
                             52.0
12-01
12-02
12-03
19,300
16,800
15,700
13.4
11.7
10.9
26.0
29.0
40.0
59.0
88.0
55.0
                                44

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During the winter the lagoons froze over and some of the neighborhood
children went riding mini bikes on the ice.   Fencing the facility site  was
not sufficient to prevent access.   The Lot  Owners decided that  there should
be an additional fence erected around the lagoons as soon as  possible.

By June 30, 1971 there were twenty-three homes discharging into the lagoon.
This flow coupled with surface run-off had  caused sufficient  accumulation of
liquid to enable irrigation to be applied to the hay crop the week of
July 18, 1971.

Operating procedures for the lagoon-irrigation facilities were  designed for
maximum flexibility.  Descriptions of these procedures which  follow are
keyed to Figure 11.  Under normal conditions the influent wastewater,  after
passing through the parshall flume, went first to the surge tank (valve #1
open).  When the surge tank reached a set level, pumping unit #1 pumped the
surge tank contents to lagoon 1.  During power outages or peak  flows which
exceeded the 4-inch line capacity, the influent automatically bypassed to
the lagoon via bypass #1.  Lagoon 2 was designed for use during periods of
high flow and during the winter for prolonged storage.  The system also had
the capability for recirculation from lagoon 2 to lagoon 1 by closing  valves
#2, 3, and 4, opening valve #5, and operating pumping unit #2.   In addition,
lagoon 1 could be mixed by closing valves #2 and 4, opening valves #3  and  5,
and operating pumping unit #2.

Irrigation of the hay field could be accomplished from either lagoon 1 or
lagoon 2.  Lagoon  1 effluent could be used  (minimum depth was maintained)  by
closing valves #2  and 5, opening valves #3 and 4, and operating pumping unit
#2.  Lagoon  2 effluent could be used by closing valve #5, opening valve #4,
and operating pumping unit #2.

The non-irrigated  hay field runoff was collected, sampled and metered to the
stream via pumping unit  #4.  The volume of  runoff discharged was then used  as
the "target" volume to be sampled and metered to the  stream  from the irrigated
hay field runoff-collection tank via pumping unit #3  with valve #6 open and
valve #7 closed.   Any excess  over the target volume in  the irrigated field
runoff  collection  tank was recycled to the  sprinkler  irrigation  system by
using pumping unit #3 with valve  #6 closed  and  valve  #7 opened.

Surface runoff  continued to be a  problem due to soil  erosion into the  drain-
age ditches  around the  lagoon.  Maintenance of the  ditches became critical
and required additional  grading by the  contractor.

On January 9,  1972 a fault  in the levee  (See Figures 12, 13, 14,  15,  and
 16) around the  secondary lagoon broke and  approximately 750,000 gallons of
 irrigation liquid ran out through the break and eventually into the stream.
This  was reported promptly to the State Board of Health and  the receiving
 stream was tested for contamination.   A 5-day BOD test of the  irrigation
 liquid just prior to the break was 6.5 mg/1.   The 5-day BOD's  taken at
 selected points in the stream ranged from a high of 4.2 mg/1 at the point of
 discharge into the stream to 1.3 mg/1 1 mile downstream.  A  slight  odor was
 evident 1 mile downstream but not evident 1.8 miles downstream.
                                       45

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                                                                 700
SLOPE 2.5:1
                                                                           695
                     DRAINAGE DITCH
                 FIGURE 12. LAGOON LEVEE FAILURE
      SOIL BORING LOCATION




      AREA OF LEVEE  FAILURE




  1+1  STATION OF X-SECTION
 •^•^MMB



-675—ORIGINAL GRADE  ELEVATION

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700:
 FIGURE 13. LAGOON LEVEE FAILURE X-SECTIONS AT STATIONS
          0+00 AND 0+10
  FIGURE 14. LAGOON LEVEE FAILURE X-SECTIONS AT STATIONS
           0+20 AND 0+45
                          47

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33JL
           ^iiLf Trisfe
                           •1*150:-. :
                           .. i.,,,..: .
                                                         -M-rt~
                                              120-T>^Mfi1- -1^0--^
                                          _l..;.4-i.:_!..:.,. pwh,-,!...'...  .
                                                        _.7WiuMnl
                                             . . ._.      .     ,. TJ
0;  -•?<)•  • 40 -   - 60^-' r-Sto
  FIGURE 15. LAGOON LEVEE FAILURE X-SECTIONS AT STATIONS

            1+00 AND 1-1-50
  FIGURE 16. LAGOON LEVEE FAILURE X-SECTION AT STATION 1+65
                              48

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Investigation into the cause of the slide revealed:

1.   Irrigation of the plant effluent had been curtailed due to poor weather
    conditions and soil conditions.

2.   The lagoons were full to the point of utilizing about one-third of
    the freeboard available.

3.   Recent rains had kept the levee around the lagoon saturated.

4.   The layer of shale noted in the original core borings was removed
    by the contractor in Cell I and clay compacted in its place.   In
    the area of the levee, the contractor cut through the shale layer,
    removed the shale, and cut and constructed the levee key below that
    layer.

Soil conservation officials and the engineers observed that apparently a
second layer of shale  (soapstone) existed beneath the two lagoons that was
not revealed in core boring No. 8  (See Figure 17) taken prior to construction.
This material became saturated and very slick.  The weight of the levee and
the impounded liquid caused the entire section of the levee to slip down
the soapstone layer.  A solution to the problem proposed that a series of
drains be installed in the  soapstone  layer and in the toe of the levee.
This was deemed too costly  and a larger lagoon was built at a different
location on the plant  site.

The new lagoon was designed to provide storage of four months of flow  from
one hundred houses plus rainfall.  The lagoon had a surface area of  1.78
acres and had a total  depth of ten feet of which 2.4 feet was freeboard.
Additional irrigation  area was also recommended at that time  (See Figure 18).

Maintenance of the treatment plant proved to be much higher than anticipated
in the original design estimate.  The fact that the treatment process  was
simple did not enable  limited maintenance of the equipment.  A higher  initial
installation cost with an automated irrigation system might have resulted  in
lower overall costs.
                                      49

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i
A\\\\
 HOLE

 NO.7
         °'!
         I
HOLE

NO.8
                   710
                   705
           700
          695
                   690
                   685
SILT





SILTY-CLAY






CLAY





SHALE
      FIGURE 17. LAGOON SITE BORING LOGS
                      50

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                   GRANDVIEW LAKE
                                                                    SYSTEM
                                                                    MAIN LINE
                                                                                                   ABANDONED
                                                                                                    NON-IRRIGATET
                                                                                                     FIELD
                                      AIR RELEAS
                                      VALVE
         pvc   PARSHALL FLUME
                  2  1/2" SUCTION FROM   ^
                  PRIMARY LAGOON
ABANDONED
SURGE  TANK t
                                                                                                       ABANDONED
                                                                                                        IRRIGATION
                                                                                                         FIELD
                                                                                                            EXISTING
                                                                                                             PUMPINC
                                                                                                              UNIT
                                                                                     NEW SECONDAR
                                                                                     STORAGE  LAGOON
PROPOSED
IRRIGATION
FIELD
                                     FIGURE 18. REVISED TREATMENT PLANT LAYOUT

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                                  SECTION X

                      LAGOON  EFFLUENT  IRRIGATION DATA

As originally proposed, the  liquid from the lagoons was to be irrigated onto
a hay crop at regular intervals throughout the summer months.  A 1-acre irri-
gation field and similar-sized control field were to be utilized to determine
the amount and strength of runoff from irrigated and non-irrigated land.  No
discharge from the irrigated field was planned other than an amount equal to
that from the non-irrigated  field.  The volume of the discharge was equalized
by re-irrigation of any runoff from the irrigated field.  A partial failure
of the irrigation field crop due to flooding prohibited total operation as
originally proposed.  Additional irrigation areas were utilized as needed,
but conclusions as to the effectiveness of such application in relation to
ground slope, type of vegetation, frequency of application were drawn.

Individual applications to the 1-acre field over a 24-hour period ranged
from 15,400 gallons to 52,100 gallons or a depth of 0.57 to 1.92 inches.
The normal operating level was about 24,000 gallons or 0.88 inch.  The
period of recovery between applications varied with temperature, humidity
and wind velocity.

Total crop irrigation during 1971 was as follows:

               Month                       Gallons

               July                        15,200
               August                      31,600
               September                    7,500
               October                     14,260
               November                     2,700

                 Total                     71,260 gallons

Prior to the failure of the lagoon levee an auxiliary irrigation system was
laid out in the woods near the treatment plant.  In 1971, 74,800 gallons were
pumped onto the vegetation without any runoff to the stream.   Therefore, the
total volume of lagoon effluent discharged to the land in 1971 was 146,060
gallons.

The irrigation system was then moved in December, 1971 to another location
where vegetation was thicker than at the previous location.   Further damage
to the lagoon levee was prevented by irrigating to this area in addition to
the irrigated hay field in 1972.   Irrigation figures for 1972 are as follows:
                                     52

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               M°nth                            Gallons

               August                           400,625
               September                        676,332
               October                           52,150

                         Total                1,109,107

As noted earlier, when the new lagoon was designed it was recommended that
a larger area (5.5 acres) be used for irrigation to effectively consume the
liquid volume entering the plant.

The lezbedeza hay crop intially used was killed off by excess water, but a
fescue mixture used the second year was hardier.  It was found by the
operators that the initial application to vegetation areas far exceeded the
average load applicable without runoff to the stream.  Multiple applications
created washed areas on slopes greater than 4 to 1 and pooling in depressions
prevented any new growth.  The best area for irrigation was one which had
dense grasses and trees less than 15-feet tall.

Ideally, the frequency and intensity of application would have been no
greater than 25,000 gallons every third day at the Grandview plant due to
soil conditions.  By anticipating a rotation of irrigation areas to allow
such a schedule, the engineer could minimize runoff.  Of course, naturally-
wooded areas might utilize a greater or lesser volume of liquid per acre
due to type of vegetation, ground slope, soil type, etc.  It was the
engineer's experience that the capability for irrigating several times the
average daily irrigation volume was necessary for disposal due to weather
factors.  One acre could be used to dispose of 1,920,000 gallons  [24,000 x
1/3 (30 days) x 8 months] of liquid under ideal conditions.  However, a
design factor of 1,303,315 gallons per acre or 48-inches of liquid per year
was used in sizing the new irrigation area.
                                     53

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                                 SECTION XI

                             LABORATORY ANALYSES

During the research period of the Grandview Lake Sewage Project,  specific
laboratory tests were performed to answer the following:

     1.  What was the strength of the waste at the home pumping
         units?
     2.  What was the strength of the waste entering the plant?
     3.  How effective was the lagoon treatment?
     4.  How effective was the irrigation step in reducing the
         strength of the lagoon effluent?
     5.  How did the runoff from the irrigated field compare to
         the runoff from the non-irrigated field?

The procedures followed for testing the sewage samples conformed  to
Simplified Laboratory Procedures for Wastewater Examination, published by the
Water Pollution Control Federation (WPCF Pub.  No. 18).

Specific tests conducted on the samples collected were:

     1.  Biochemical Oxygen Demand CB.O.D.)
     2.  Suspended Solids
     3.  Orthophosphates
     4.  Ammonia-Nitrogen
     5.  Nitrite-Nitrogen
     6.  Nitrate-Nitrogen
     7.  Chemical Oxygen Demand (C.O.D.)

Evaluation of the various samples resulted in the following conclusions:

The strength of the sewage found in the home units varied widely  with unit
type.  The septic tank effluent systems had the lowest concentrations of BOD,
COD and suspended solids, but also had the most pronounced odor.   A higher
strength waste was collected at the various home units than was seen entering
the plant.  This higher strength was to be expected since no sedimentation
(septic tank) was provided prior to the pumping units.

After the levee failure, lack of aeration or recirculation and the reduced
storage capacity caused the upper portion of the primary cell to  turn septic
toward the end of the research period.  Excellent treatment was obtained by
the overall treatment sequence, as evidenced by the field runoff  comparisons,
shown in Table 7.

Although the data are limited a number of consistencies are evident.  First,
the plant influent, being a mixture of grinder-pump and septic tank effluent

                                      54

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      Location

ONSITE

Grinder-Pumps

Septic Tank Effluent

PLANT INFLUENT

LAGOON 1 EFFLUENT

FIELD RUNOFF

Irrigated

Non-Irrigated
                                   TABLE 7

                             ANALYTICAL SUMMARY
Number of
 Samples
Composite
 or Grab
Average Concentration,  mg/1
BOD   COD    SS   P04  N(l)
3
1
5
3
3
3
G
G
4C;1G
G
G
G
360
110
216
128
9
11
560
190
413
275
49
59
470
95
170
140
8
48
31
22
40
32
6
NIL
41
44
39
22
15
6
(1) Nitrogen data represent sum of NH3, N02 and NO^ results, expressed as N.
                                      55

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pump flows, generally has measured pollutant concentrations intermediate
between the two sources.  Secondly, the lagoon effluent does demonstrate some
treatment efficiency when compared to the influent, including some nutrient
reduction.  Finally, the runoff from the irrigated hay field was of somewhat
better quality than the non-irrigated field with respect to BOD, COD and
suspended solids.   An increase in nutrients appears to exist, but when
compared to the plant influent, a significant reduction in nutrients appears
to take place during the treatment sequence.

A complete list of analytical results is given in Table 8.

Even the limited scope of the testing on this project confirmed that irriga-
tion of treatment plant effluent was an effective method of disposing of
domestic sewage.
                                      56

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                                  TABLE 8

                              ANALYTICAL DATA
                                   (1972)
Location (T
(#)
1


2
3




4


5


6


Sample
) Date
10/17
10/17
11/1
11/1
9/5
9/14
11/30
12/7
12/11
9/5
10/17
11/1
7/23
10/17
11/1
7/23
10/17
11/1
Type
(CorG)
G
G
G
G
G
C
C
C
C
G
G
G
G
G
G
G
G
G
Parameter Measured (Concentrations in mg/1)
BOD5
690
180
210
110
305
185
310
100
180
170
95
120
3
9
16
4
19
10
COD
707
460
508
191
533
457
462
230
382
337
207
282
58
33
56
62
61
44
SS
1080
145
175
95
268
136
264
80
102
116
140
165
11
6
6
7
60
78
m4
23
32
37
22
28
59
48
32
34
27
28
42
NIL
2.5
16
NIL
NIL
NIL
N03-N
7
7
5
4
1.5
9
0.2
4
0.3
1
2
5
-
1.8
18
-
1.8
4
N02-N
NIL
NIL
NIL
NIL
NIL
1.0
NIL
NIL
NIL
NIL
NIL
NIL
_
NIL
NIL
_
NIL
NIL
NH--1*
70
17
18
40
16
47
45
34
39
19
20
19
0.7
0.6
8.0
0.8
0.2
5.0
Location:   1 - Grinder Pumps
           2 - Septic Tank Effluent Pumps
           3 - Plant Influent
           4 - Lagoon 1 Effluent
           5 - Irrigated Field Runoff
           6 - Non-Irrigated Field Runoff
                                     57

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                                 SECTION XII

                            COSTS AND DISCUSSION
One of the anticipated results of the Grandview Lake Research and
Demonstration Project was to provide inexpensive sewers to rural areas.   It
appears that a price of about $600 to $1,500 for each individual grinder-pump
can be anticipated.  The engineer originally felt that a unit could be pro-
duced for less than $500.  Since present financing limitations per customer
in sparsely populated areas are such that only about one-third of the borrowed
monies can realistically be applied to a grinder-pump unit, i.e., two-thirds
would be applied to system piping and treatment facilities, this early esti-
mate would have enabled greater application of the pressure sewer approach.
There is the possibility that free market conditions may force the price of
the grinder-pump units down.  This would make future projects more feasible.

It was found that a great amount of engineering time, especially in the field,
and close construction inspection was needed during installation and start-up
of the system and home units.  It is anticipated that as contractors become
better acquainted with pressure sewer systems that this would be minimized.

The impact of the sewer system being available to the lot owners was best seen
in two indicators; the ratio of permanent residences to part-time residences
and the purchase price of lots before and after the pressure sewer install-
ation.  When the system operation was begun in November 1970, there were 22
houses that were occupied on a full-time basis and 36 on a part-time basis.
By June 13, 1972, the number of part-time occupancies was negligible and 100
permanently-occupied homes were anticipated in the area served by the initial
system.  During the same period of time the value of the lots had increased as
much as 45 percent.  The reluctance of potential buyers to locate where sewer
facilities were not available was overcome by the pressure sewer system.

The construction cost summary for the pressure main is presented in Table 9.
In addition, the treatment facility, including the lift station capital cost
was $32,142.  Therefore, the total capital cost per home would be the sum
of the pressure main and treatment facility, divided by the number of homes
served, added to the cost of the onsite facility of each homeowner.   The
approximate costs of the various units employed in the study are given in
Table 10.  Since the number of operating units varied throughout the study
and since a number of original units were replaced during the course of the
project, an exact average cost is not easily computed.  For example, if the
original 58 homes were chosen, the average cost of the main and treatment
facilities per home was $1,166, plus the onsite cost.  If the ultimate pro-
jection of 100 homes were chosen, the average cost drops to $676, plus the
onsite facilities.


                                      58

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                                   TABLE 9

                        PRESSURE SEWER COST BREAKDOWN
         Item


5-inch PVC (SDR 26)

3.5-inch PVC (SDR 26)

3-inch PVC (SDR 26)

2-inch PVC (SDR 26)

Blacktop Road Repair

Manual Air Release Valves

Automatic Air Release Valves

Mainline Gate Valves § Boxes
Quantity
Unit
Cost
Total
635 ft
11,475 ft
14,155 ft
1,230 ft
40 ft
6
4
2
$2.00/ft
1.10
1.10
0.90
3.00
125.00 ea.
200.00
100.00
$ 1,270
12,622
15,571
1,107
120
750
800
200
                                              Total Cost*   $32,440
*Bid cost, not including $1,000 vacuum collection station.
 Actual cost, including vacuum station, was $33,044.
 Final cost including additional items such as  an extension  of  the main,
   line relocation, county blacktopping and rock excavation  was $35,491.
                                    59

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                                               TABLE 10

                                APPROXIMATE HOME UNIT COST COMPARISON
       Type  of Unit


Septic Tank Effluent  Pump
  and  Tank  (3)

Hydromatic  GP

Environment  One GP

Tulsa  GP

Moyno  GP

Flushing Unit with
  1000 gallon Tank
Delivered
Cost(l)
670
920
950
600
600
750
Cif requiret
ft. of 1-inc
Installation
Cost
200
200
200
200
200
450
.).«.. 11 »c
:h PVC service
Service Line §
Connection Cost (2)
160
160
160
160
160
200 (4)
:illary items for comple
line, curb cock, and al
Total Cost
1030
1280
1310
960
960
1400
te system,
1 other
(2)  serviceline
(3)  When new installation, approximately $400 must be added for septic tank
(4)  Larger (1.5-inch)  service lines generally required for flushing units.

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Due to the experimental nature of the project,  an unusual amount of public
relation work had to be done on the Grandview project.   The engineer was very
fortunate to have a Utility Board composed of engineers and businessmen
familiar with research and development projects.   They understood that every-
thing was not going to function perfectly from the start.  They did an
excellent job of explaining to the homeowners that problems would arise, but
that they would be dealt with as soon as possible.  Generally, the attitude
of the homeowners was very good.  They realized that the "bugs" had to be
worked out of the system and there would be some inconveniences.  The alter-
native to the project, septic systems leaking into yards and the lake, no
doubt was an influencing factor in their attitude.

The initial concept of the engineer was to develop a fractional horsepower
grinder-pump unit with parts that were readily available to the homeowner in
the event of malfunction.  The horsepower was to be kept to a minimum to help
reduce the homeowner's electrical bill.  It became very evident during the
project that the homeowner was neither interested in a low electric bill
nor   able to service the unit himself.  He simply wanted a maintenance-free
sewer system.

The community's primary goal was to obtain a functional sewer system.  The
research project funds provided a start toward that goal, but were never
intended to be limited to that use.  Knowledge was gained from the failures
as well as the successful parts of the project.
                                      61

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                                SECTION XIII

                                 REFERENCES

1.  Waller, D. H., "Experience with Grinding and Pumping of Sewage from
    Buildings," Tech. Memo Nos. 3 and 3A, ASCE Project  (1967).

2.  Farrell, R. P., Anderson, J. S., and Setser, J. L., "Sampling and
    Analysis of Waste Water from Individual Homes," 67-MAL-3, General
    Electric Company for ASCE Combined Sewage Separation Project (1967).

3.  Linaweaver, F. P., Jr., Geyer, J. C. and Wolff, J.  B., "Final and
    Summary Report on Residential Water Use Project," Johns Hopkins
    University (1966).

4.  Tucker, L. S., "Sewage Flow Variation in Individual Homes," Tech.
    Memo.  No.  2,  ASCE Combined Sewage Separation Project (1967).
                                  62

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                                 SECTION XIV

                                PUBLICATIONS
1.   Rees,  S.  M.,  "Wastewater Disposal Plan to Protect Recreational Lake,"
    Public Works, 103,  No.  4, pp.  88-91 (1971).

2.   Sanson, R.  L.,  "Design Procedure for a Rural Pressure Sewer System,"
    Public Works, 105,  No.  10, pp.86-87 (1973).

3.   Hendricks,  G. F., and Sanson,  R. L., "Pressure Sewer Design Procedure,"
    Water S Sewage Works, 122, No. 11, pp. 53-54 (1973).

4.   Hendricks,  G. F., "Pressure Sewer System and Treatment at Grandview
    Lake, Indiana," Proceedings of Ohio Home Sewage Disposal Conference,
    Columbus, Ohio, January 79-31, 1973.

5.   Hendricks,  G. F., "Pressure Sewer System and Treatment, Grandview
    Lake, Indiana," Paper presented to Annual Meeting of American Society
    of Agricultural Engineers, Pullman, Washington, June 27-30,  1971.
                                      63

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                               SECTION XV

                               GLOSSARY
English units
     (    )          X

Length

     mile
     foot
     inch  (")

Area

     acre

Volume

     gallon

Mass

     pound

Volume rate of flow
     gallon/day (GPD)
     gallon/minute (GPM)

Volume loading rate
     gallon/acre

Pressure
Conversion factor
     C      )
 1.609
 0.305
25.4
 0.404
 3.786
 0.454
 0.0038
 0.0631
 0.0094
     pound(f)/square inch(psi)    6.895
Power
     horsepower
 0.7457
                           Metric
                            (  )
                               kilometer
                               meter
                               millimeter
                               hectare
                               liter
                               kilogram
                               meter /day
                               liter/second
                               meter /hectare
                           kilopascal
                               kilowatt
                                    64

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                                  TECHNICAL REPORT DATA
                           (Please read Instructions on the reverse before completing)
 REPORT NO.
 EPA-600/2-75-072
            3. RECIPIENT'S ACCESSIOWNO.
 TITLE AND SUBTITLE
                                                          5. REPORT DATE
 ECONOMICAL RESIDENTIAL PRESSURE  SEWER SYSTEM
 WITH  NO EFFLUENT
                                                           December 1975 (Issuing  Date)
            6. PERFORMING ORGANIZATION CODE
 AUTHOR(S)
                                                          8. PERFOBMING ORGANIZATION REPORT NO.
 Gerald F.  Hendricks and Stephen M.  Rees
 PERFORMING ORGANIZATION NAME AND ADDRESS
 SIECO,  Inc., Columbus, Indiana  (for)
 Grandview Lot Owners Association
 RR6  - Grandview Lake
 Columbus, Indiana  47201
            10. PROGRAM ELEMENT NO.
             1BB035/21-ATC/004
            115«Qt*Btte8CX/GnANT NO.

             S801041
2. SPONSORING AGENCY NAME AND ADDRESS
 Municipal Environmental Research Laboratory
 Office of Research and Development
 U.S.  Environmental Protection Agency
 Cincinnati, Ohio  45268	
            13. TYPE OF REPORT AND PERIOD COVERED
            Final - 4/69 to 11/72	
            14. SPONSORING AGENCY CODE
             EPA-ORD
5. SUPPLEMENTARY NOTES
6. ABSTRACT

An economical pressure sewer system with no polluting  effluent was designed,
constructed, and monitored  for effectiveness.  The  elimination of groundwater
infiltration and restrictive elevation tolerances associated with a conventional
gravity sewer system enabled this type of sewer  system to be installed and  to
function economically.  The treatment process, aerobic and anaerobic  lagoon storage
with subsequent irrigation  of the effluent, yielded no more than normal  volume of
runoff.

Operational problems with the pressure system resulted from inefficient  home grinder-
pump units.  These problems were greatly reduced when  commercially manufactured home
units became available.  The treatment process functioned as anticipated.   Because of
the new sewer system, summer homes become year around  residences and  new home con-
struction exceeded expectations.  As a result, the  initial irrigation area  proved
inadequate for handling the actual flows and additional irrigation area  was made
available at a later date.
                               KEY WORDS AND DOCUMENT ANALYSIS
                  DESCRIPTORS
                                              b.lOENTIFIERS/OPEN ENDED TERMS
                             COSATi Field/Group
 Sewers
 Sewage
 Sewage treatment
 Sewage disposal
 Pressure sewers
 Lagoons
 Effluent irrigation
13B
18. DISTRIBUTION STATEMENT
 RELEASE TO PUBLIC
                                              19. SECURITY CLASS (This Report)
                                                    UNCLASSIFIED
                           21. NO. OF PAGES
                                  73
20. SECURITY CLASS (Thispagt)
      UNCLASSIFIED
                                                                         22. PRICE
EPA Form 2220-1 (9-73)
                                             65
                                                               OUSGPO: 1976 — 657-695/5358 Region 5-11

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