EPA
     ill Protection
Officf of      Industrial Environmental Research
Research and    Laboratory
Development    Research Triangle Park, North Carolina 27711
                                          EPA-b'OU
            MAGNESIA  SCRUBBING
            APPLIED TO A COAL-
            FIRED POWER  PLANT
            Interagency
            Energy-Environment
            Research and Development
            Program Report

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                       RESEARCH  REPORTING SERIES
Research reports of the Office of  Research and Development, U.S.
Environmental Protection Agency, have been grouped into seven series.
These seven broad categories were  established to facilitate further
development and application of environmental technology.  Elimination
of traditional grouping was consciously  planned to foster technology
transfer and a maximum interface in  related fields.  The seven series
are:

     1.  Environmental Health Effects Research
     2.  Environmental Protection  Technology
     3.  Ecological Research
     4.  Environmental Monitoring
     5.  Socioeconomic Environmental Studies
     6.  Scientific and Technical  Assessment Reports (STAR)
     7.  Interagency Energy-Environment  Research and Development

This report has been assigned to the INTERAGENCY ENERGY-ENVIRONMENT
RESEARCH AND DEVELOPMENT series.   Reports in this series result from
the effort funded under the 17-agency Federal Energy/Environment
Research and Development Program.  These studies relate to EPA's
mission to protect the public health and welfare from adverse effects
of pollutants associated with energy systems.  The goal of the Program
is to assure the rapid development of domestic energy supplies in an
environmentally—compatible manner by providing the necessary
environmental data and control technology.  Investigations include
analyses of the transport of energy-related pollutants and their health
and ecological effects; assessments  of,  and development of, control
technologies for energy systems; and integrated assessments of a wide
range of energy-related environmental issues.

                            REVIEW NOTICE

This report has been reviewed by the participating Federal
Agencies, and approved for publication. Approval does riot
signify that the contents necessarily reflect the views and
policies of the Government, nor does mention of trade names
or commercial products constitute endorsement or recommen-
dation for use.
This document is available to the public through the  National Technical
Information Service, Springfield, Virginia  22161.

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                                   EPA-600/7-77-018

                                   March 1977
        MAGNESIA SCRUBBING

              APPLIED  TO

   A  COAL-FIRED POWER  PLANT
                     by

               George Koehler

    Chemico Air Pollution Control Company
               One Perm Plaza
         New York, New York 10001


           Contract No. 68-02-1870
        Program Element No. EHB528
     EPA Project Officer:  C.J. Chatlynne

 Industrial Environmental Research Laboratory
   Office of Energy, Minerals, and Industry
      Research Triangle Park, NC 27711
                Prepared for

U.S. ENVIRONMENTAL PROTECTION AGENCY
      Office of Research and Development
            Washington, DC 20460

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                     ABSTRACT

     A full-size demonstration of the magnesia wet-scrubbing
system for Flue Gas Desulfurization (FGD)  was conducted on
a coal fired utility boiler.  The system was designed to de-
sulfurize one-half the flue gas from a 190 MW rated capacity
generating unit firing 3.5% sulfur coal.  The FGD installa-
tion was equipped with a first-stage wet scrubber for parti-
cle emissions control followed by the magnesia unit.
     Twenty-eight hundred hours of operation were logged at
the generating station, and the FGD system's ability to re-
move 90% of the inlet S02 was shown.  The particle control
capability of the unit was also demonstrated by reducing
particle emissions to less than 0.01 gr/SCFwhen the unit
was operated in series with an electrostatic precipitator.
In a test program using only the wet scrubbing unit for par-
ticle emissions control a collection efficiency of 99.6%
was achieved.
     Magnesia was regenerated and recycled successfully.
The SO- produced during regeneration was used to manu-
facture commercial grade sulfuric acid which was marketed.
Correlations were developed to determine SO, removal for
varying boiler loads and fuel sulfur content, and to control
regeneration of acceptable alkali.  Several other studies of
the process technology and process chemistry were undertaken
as part of the work.
                      111

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            TABLE  OF  CONTENTS

                                                 PAGE

1.0  Summary                                      1
     1.1  Operational Effect of Design            5
           Variation From the Oil Fired Case
     1.2  Effect Of Process Chemistry             7
           Variations on System Performance

2.0  Introduction & Background                    9

3.0  Process Description                          16
          3.0.1  Facility Description             19
          3.0.2  Pollution Abatement System       21
                  Description
     3.1  Detailed Process Description - FGD      25
           System
          3.1.1  Particle Removal                 25
          3.1.2  SO- Removal                      31
     3.2  Magnesia Regeneration System            34
     3.3  Acid Plant                              40
          3.3.1  Acid Plant Modifications         41'
          3.3.2  Acid Production                  44

4.0  Pollution Abatement System Performance       48
     4.1  Development Test Program                50
          4.1.1  October 1974 Details             58
          4.1.2  November 1974 Details            58
          4.1.3  December 1974 Details            60
          4.1.4  January 1975 Details             61
     4.2  Utilities Consumption                   62
     4.3  MgO Consumption                         62
          4.3.1  MgO Losses During Preliminary    65
                  Operations
     4.4  MgO Regeneration - Inventory            66
     4.5  Post Operation FGD System Inspection    69
          4.5.1  1st Stage Piping                 70
          4.5.2  2nd Stage Piping                 74
          4.5.3  Corrosion of Stainless Steel     74

5.0  Performance Test Results                     76
     5.1  Particulate Emission                    76
     5.2  SO  Emissions                           78
     5.3  Particle Size Measurements              82
     5.4  Coal Analysis                           82
                      IV

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            TABLE OF CONTENTS
                                                  PAGE

 6.0  Process  Chemistry                            85
      6.1  1st Stage Operation                     85
      6.2  Process  Chemistry                       88
           6.2.1 Absorber Reactions               89
           6.2.2 Formation of Oxysulfates         90
      6.3  Magnesium Sulfite Chemistry             91
           6.3.1 Conditions Governing the         91
                   Formation of Magnesium
                   Sulfite Hydrates
           6.3.2 Dehydration of Magnesium Sulfite 93
                   Hydrates
           6.3.3 Mass  Spectroscopy of the Two     95
                   Hydrates of Magnesium Sulfite
                   vs.  Temperature
      6.4  Pulverization                           96

 7.0  Correlation of Process Data                  99
      7.1  SO- Removal                              101
           7.1.1 First Stage S02 Absorption       101
           7.1.2 Effect of Pulverization of       102
                   Regenerated MgO
           7.1.3 Reduction in Activity of         106
                   Magnesia
      7.2  Centrifuge Operation                    110
      7.3  Dryer Operation                         113
      7.4  Calciner Feed Rate                      113

 8.0  Data                                         120
      8.1  Monthly  Average Operating Conditions    120
      8.2  Data Listings                           120

 9.0  List of  Publications                         134

10.0  Conversion From English To Metric Units      137

 Appendix I -  Post  Operation Inspection Report     138

 Appendix 2 -  Thermal Dehydration of Magnesium     153
               Sulfite  Hydrates - Using Thermo-
               Analytical Techniques

 Appendix 3 -  Mass  Spectrometric Study of the      201
               Thermal  Degradation of MgSO-j.3H~0
               & MgS03.6H20

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                 TABLE OF CONTENTS

                      FIGURES
                                                  PAGE

1    Two Stage Scrubber/Absorber Vessel            17
2    FGD Gas Flow Schematic - Dickerson No.  3 -    18
      PEPCO
3    The Dickerson Regenerative Wet Scrubbing      22
      System - Schematic Process Flow Diagram
4    PEPCO Regenerative Wet Scrubbing System -     26
      Process Flow Diagram
5    Magnesia Regeneration System                  35
6    Sulfuric Acid Plant - Process Flow Diagram    43
7    Tail Gas Scrubbing System - Process Flow      46
      Diagram
8    Effect of Pulverization on S02 Efficiency     97
9    Process Data Flow Diagram                     100
10   SO, Removal Efficiency vs. Time               104
11   Effect Of MgO Particle Size on S02 Removal    107
      Efficiency
12   Observed vs. Predicted S02 Removal Efficiency 108
13   Effect Of Centrifuge Feed Rate on Separa-     111
      tional Efficiency
14   Centrifuge Operation - Ib/min Solids          112
      Separated vs. Feed Rate
15   Comparison of PEPCO and Boston Edison Dryer   114
      Operation
16   Dryer Operation - Outlet Gas temperature vs.   115
      % Dry Solids
17   Comparison of MgSO3 Oxidation In Dryer        116
18   Calciner Operation - Effect Of Feed Rate On   117
      MgS03 In Product
                      VI

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                 TABLE OF CONTENTS

                                                  PAGE

                    TABLES

1   Pertinent Data On Boiler Design,  Operation     20
     and Atmospheric Emissions
2   PEPCO Regenerative Wet Scrubbing  System -      27
     Stream Properties and Composition
3   Wet Scrubbing System - Equipment  List          28
4   Magnesia Regeneration System -  Stream          36
     Properties and Composition
5   Calciner Product - Dry Screen Analysis         39
6   Sulfuric Acid Unit Feed Gas Composition        42
7   Tail Gas Scrubbing System - Stream             47
     Properties and Composition
8   Performance Test Designations                  53
9   Summary Of Operations FGD System  -             55
     Performance Test Phase
10  Summary Of Operations Calciner  System -        57
     Performance Test Phase
11  Utilities Consumption - FGD System             63
12  MgO Makeup - FGD System                        64
13  Inventory Summary By Week - FGD System         67
14  Inventory Summary By Week - Regeneration       68
     System
15  Operating History - FGD System                  71
16  Particle Emissions Test Results - FGD System   77
17  Estimate Of Electrostatic Precipitator         79
     Efficiency
18  SO  Emissions Test Results - FGD  System        80
19  Removal Efficiency For Particle Size Ranges    83
20  Coal Analyses - Composite To Bunker #3         84
21  Chemical Composition At Various Streams In     86
     The First Stage - Fly Ash Removal System
22  Properties Of Different Fraction  Of PR-289     98
23  S0~ Removal In First Stage                     103
24  Wet Screen Analysis of MgO Belt Samples        105
25  Manufacturer's Analysis of Magnesia            109
     Shipped To Dickerson Station
26  Size Distribution Of Dryer Products            119
27  Comparison Of Boston and PEPCO  size Range      119
     Averages
28  Operating Conditions For The FGD  System -      121
     Monthly Data Averages
29  Stream Compositions For The FGD System -       122
     Monthly Data Averages
30  Operating Conditions For The Regeneration      123
     Unit - Monthly Data Averages
31  Stream Compositions For The Regeneration       124
     Unit - Monthly Data Averages

32  Run Dates and Data Listings                    125
                     vn

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                TABLE OF CONTENTS
                  PHOTOGRAPHS

3-2    Centrifuge Case
3-5    Centrifuge Plow - Failed
3-11   Centrifuge Plow - Normal
4-1    Dryer
4-3    Bearing Support - Dryer Feed Screw
4-6    Dryer Burner Block Refractory
10-7   2nd Stage Venturi Throat
10-10  2nd Stage Venturi Throat
                                                  PAGE
151
151
151
151
151
151
152
152
                     Vlll

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                1.0   EXECUTIVE  SUMMARY
      The*Chemico-Basic magnesia slurry SO- recovery process
for control of sulfur oxides emissions from fossil fuel
fired utility boilers has been demonstrated on an oil fired
boiler (The Magnesia Scrubbing Process As Applied To An Oil
Fired Boiler, EPA 600/2-75-057).  This process, with some
modifications developed during early operations in New England,
was next installed on a coal fired boiler at Potomac Electric
Power Company's Dickerson Generating Station as a system to
control both particle and sulfur dioxide emissions from the
plant.  The regeneration and SO, recovery steps of the process
continued to be carried out at the Environmental Protection
Agency's calcination facility at Essex Chemicals' Rumford Acid
Plant in Rhode Island, which had originally been constructed
for the New England S02 Control Project.
      Major distinctions between these two FGD units are divided
into process design variation and process chemistry differences.
In the former category the principal variations between the
design of the previously reported oil fired application and
this coal fired boiler system were:
      A)   The addition of a first stage venturi scrubber
          for particle control only (no alkali is added
          to this stage).  Flue gas exiting this first
          stage is lowered in temperature to near the
          adiabatic saturation point through the normal
          transport mechanisms.
      B)   Magnesia alkali added to the second stage for
          SO- control is slurried with centrate returned
          from the centrifuge instead of process water.
          Since gas entering the second stage is saturated
          with water vapor little or no evaporation takes

   *Wherever the term '?Chemico"  is  referred to in this
    report,  the term "Chemico Air Pollution Control
    Company" shall be substituted therefore.

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         place; thus it is possible to eliminate
         fresh water inputs to this stage.
     C)  The use of a co-current, rather than a
         counter current dryer to dry the centri-
         fuge cake.  This design eliminates at least
         one problem encountered with the counter-
         current design used in oil fired application.
         Dust exiting with the dryer off-gas can be
         separated and fed directly to the dryer pro-
         duct discharge without adding the pneumatic
         conveying equipment necessary with counter-
         current units.
     D)  The use of "wet" fan after the two-stage
         scrubber unit to provide the induced draft
         for the venturies instead of a hot, forced
         draft type.  An important element of the pro-
         gram was the taking of flue gas containing coal
         fly ash directly from the boiler, use of the
         "wet" fan eliminated the erosion problem associated
         with dry fans handling dirty flue gas and took
         advantage of the lowered temperature and volume
         handled after the scrubbers.
     The major difference in process chemistry between the
two plants was the production of the magnesium sulfite hexa-
hydrate in this coal fired boiler application rather than
the magnesium sulfite trihydrate produced during operations
at the oil fired generating plant.  Processing of the hexa-
hydrate proved similar in many cases, to the experiences
encountered when processing the trihydrate.
     Another process chemistry difference was the evidence
that magnesium oxysulfates were formed, sometimes in large
quantities, during the slaking of MgO with centrate.  This
resulted in a subsequent reduction in SC>2 removal efficiency.
                      - 2 -

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     Because of an overlap with the operations of the oil
fired station the regeneration plant was not available to
the Dickerson facility when the FGD system was ready for
its inaugural operation.  The lack of a regeneration faci-
lity plus problems discovered during the start up period
limited the initial PEPCO operations to less than 1000 hours
in the nine months period between September 1973 and June
1974.
     On July 1, 1974 when the Rumford facility became avail-
able, an operating and development program was initiated
at PEPCO's Dickerson Station.  In the next six months another
1790 hours of operation were achieved despite a number of
new problems.  All major objectives were completed during
the period:
     1)  Operations were initiated using regenerated
         MgO.
     2)  Particle removal efficiency of 99%+ was
         verified.
     3)  S02 removal efficiency was measured, improved
         and verified at 90%.
     4)  Operating conditions for continuous running
         were established, with emphasis on MgO slurry
         mixing, control and makeup.
     5)  MgO loss points were discovered and corrected.
     6)  An operations evaluation program was established.
     7)  Material balance measurements were made.
     8)  The SO2 removal correlation developed in the
         previous study was improved to include the
         effect of regenerated MgO properties.
     9)  Preliminary correlations were developed to
         define operating variable influence on dryer
         and centrifuge system performance.
                      - 3 -

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     10)  Laboratory investigations of fundamental
          system properties were continued.
     Some important objectives were only partially attained
because of a number of shut-downs in the latter period which
limited the time available for operation.  Thus, a long dura-
tion run was not realized.  The longest uninterrupted runs
were a twelve day continuous period in October and another
of eleven days in December.  Despite these limited operations
two recycles of the magnesium oxide inventory were achieved
during the program.
     While a number of causes contributed to the interrup-
tions the major "shut-down" problems was deterioration of
the piping in the first and second stage recycle loops of
the FGD plant.  In the second stage extensive corrosion had
occurred in the unprotected steel pipe at some time during
the preliminary operations.  In the first stage recycle pipe,
which was rubber lined, a number of failures occurred which
were attributed to the supply of off-specification pipe
and fittings during construction.
     After a piping replacement program and other repairs
to the FGD plant had been completed in preparation for a
demonstration run, the project was terminated when a rou-
tine overhaul of the power plant's generator system in
January 1975 revealed a defect in the turbine case.  The
resultant five month outage required for repair of the tur-
bine extended past the close-out date of the E.P.A. con-
tract for access to the acid plant and operation of the re-
generation facility, thus forcing the end of the project.
     Despite the limited operations and lack of extended
operating data a number of conclusions concerning the oper-
ability at the plant can be gathered from the information
that was obtained.
                       -  4  -

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1.1  OPERATIONAL EFFECT OF DESIGN VARIATION FROM THE
     OIL FIRED CASE
     A)   Particle removal efficiency for both the case
         in which gas was first cleaned in an electro-
         static precipitator and the case where dirty
         flue gas was taken directly from the boiler
         exceeded process guarantees.   With the elec-
         trostatic precipitator in the circuit an aver-
         age outlet loading of 0.002 gr/ACF was attained
         with the unit handling its full rated capacity.
         When treating dirty flue gas an average removal
         efficiency of 99.6% was obtained at full load
         operation.  The outlet loading from the scrub-
         ber system for this case was 0.011 gr/ACF.
     B)   Slurrying magnesia feed with centrate posed some
         problems.  It appears that part of the MgO feed
         is complexed as a magnesium oxysulfate.  This
         resulted in the formation of lumps and gels which
         plugged feed lines in the early operations.  This
         problem was solved by:
         1)  Providing an intensive mixer between the
             MgO feeder and slurry tank.
         2)  Slurrying the MgO feed with the entire
             recycle centrate stream to reduce concen-
             tration.
         3)  Adding a steam sparger to the slurry tank
             to heat the slurry to 180°F.
         These fixes diminished the problems to a level
         that  allowed more routine system operation.
         A reduction in S02 removal efficiency was also
         noted over a period of time during which virgin
         MgO was the major part of the feed.  Continued
                      -  5  -

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    operations showed a recovery in efficiency
    when using regenerated MgO.
    Performance tests for S02 removal run on
    recycled MgO gave an average 90% and 93.9%
    S02 removal efficiency with the scrubber
    operating at full rated capacity with S02
    inlet concentrates of 771 PPM and 1418 PPM,
    respectively.
    An explanation of the reduced efficiency when
    using virgin MgO is the more rapid formation of
    the complex, magnesium oxysulfate, with this
    more reactive material.
C)  The co-current dryer system used in the PEPCO
    operation had a higher efficiency than the unit
    used in the oil-fired case.  Extensive modifica-
    tions of the counter-current dryer/ to prevent
    material sticking to the walls,included elimina-
    tion of most of the internal lifters.   This would
    account for the higher co-current efficiency.
    A number of instances were encountered during the
    PEPCO operations in which centrifuge cake feed
    was reported as sticking to the dryer walls.
    This was corrected several times "on the run" by
    reducing load.  There were some cases where large
    deposits in the dryer resulted in a temporary shut-
    down.
    It should be noted that the dryer had been designed
    to accept a set of chains, but these had not been
    installed pending the outcome of the development
    test work.   Because of the unanticipated shut-down
    of the entire operation this potential was not
    demonstrated.
                 - 6 -

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         Dryer product from the PEPCO operation also
         proved more difficult to handle in this re-
         generation step, and resulted in a forced cut-
         back in calciner feed rate to one half that
         obtained on the oil fired application.  The
         reduced feed rate was correlated with a higher
         percentage of fines in the PEPCO dryer product,
         with only 22% as + 25 mesh in the PEPCO dryer
         product versus 58% in the same mesh size for
         the Boston Edison dryer product.
     D)   The wet fan performance and service was
         excellent.  There were no signs of deterioration,
         wear or corrosion after all operations comple-
         tion in either E.S.P. treated or untreated flue
         gas modes.
1.2  EFFECT OF PROCESS CHEMISTRY VARIATIONS ON SYSTEM
     PERFORMANCE
     A)   Production of magnesium sulfite hexahydrate
         rather than magnesium sulfite trihydrate resulted
         in little or no relief from the problems of "wet"
         centrifuge cake encountered in the oil fired appli-
         cation.
         In normal operations, after attaining equilibrium,
         the centrifuge cake contained a mix of 82% as
         hexahydrate, 18% as trihydrate for its magnesium
         sulfite component.  Materials handling problems
         were solved, as in the oil fired case, by design-
         ing the system to take any consistency of the cen-
         trifuge cake.
         Improvements were made in redesigning the centri-
         fuge discharge chute with a vertical wall on the
         solids discharge side of the machine and by lining

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    the chute with plastic to overcome the sticking
    tendency of the cake.
B)  Processing problems resulting from the formation
    of the complex S04Mg MgO H20 have been described
    in A-2 above.  Laboratory experiments indicate
    that this material is formed more readily when
    slaking a highly reactive magnesia (as virgin
    MgO grade used in this operation).  Performance
    improves when the feed is composed of a high per-
    centage of recycled MgO.  It appears that the
    complex formation occurs during the step
    M9°(s) + H20 (1)	>Mg (OH) 2  (s)
    as subsequent laboratory tests showed no oxy-
    sulfate formation when the starting material was
    magnesium hydroxide.
C)  Other Findings
    Explanations were developed for the contradictions
    in the findings of various researchers on the
    thermographic analysis of the magnsium sulfite tri-
    and hexa-hydrates.  It was shown that the dehydra-
    tion can be characterized as one-step in an open,
    non-equilibrium process whereas in a  closed,  equi-
    librium process it proceeds at the expected two
    step dehydration.  No evidence was found for the
    existance of any lower hydrate.
    This work led to a simple and accurate method of
    analysis for the ratio of the two hydrates using
    thermogravemetric analysis (T.G.A.) techniques.
                  - 8 -

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       2.0   INTRODUCTION AND BACKGROUND

     The Chemico-Basic magnesia slurry process for S02
control had been developed in laboratory and pilot plant
studies over a number of years.  The first prototype plant
employing this system was intalled on an oil fired boiler
at Boston Edison Co.'s Mystic Station on a program (New
England SO- Control Project) that spanned four years from
the signing of the contract to the completion of the test
work in July 1974.
     Concurrently with the development of the "New England
Project" Chemico pursued other potential applications for
this efficient flue gas desulfurization method.
     Applications were investigated that would further
demonstrate the broad range of its use, particularly the
advantages in those areas where a regenerable, non sludge-
producing sulfur oxides control method was mandated.
     Simultaneously, forward thinking utilities, such as
Potomac Electric Power Company, were also investigating a
number of process schemes  that would provide a means of con-
trol of their sulfur oxides emissions in order to satisfy the
new limitations being imposed by municipal, state and Federal
governments.  A principal criterion in selection of the pro-
cess for control of the recognized pollutants was the econo-
mics associated with the alternate of a low sulfur content
fuel supply.
     In late 1970 Chemico submitted a proposal  to PEPCO
for a prototype demonstration plant using the Chemico-
Basic process.  The prototype  location was  set  for PEPCO's
Dickerson generating station site approximately 35 miles
northwest of Washington, D.C.  in Montgomery County,  Maryland.
                      - 9 -

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This site consists of 1000 acres in a rural area  (but with
suburban expansion from Washington developing within a few
miles of the plant) bordered on the west by the Potomac
River and the Chesapeake and Ohio Canal National Historic
Park.  The site had also been planned by PEPCO as the loca-
tion of a 1700 MW expansion of generating capacity which
was to be coal fired in accordance with company considera-
tions for a balance of fuel types.  PEPCO had successfully
developed methods for adequate disposal of its fly ash from
the Dickerson Station; therefore, a major consideration for
future planning was the selection of a process for sulfur
oxides control which would be acceptable at this environ-
mentally sensitive site.  Regenerable processes were a major
candidate because of the complexity that would be added to
operation of the power plant by the requirement to dispose
of the larger volume of residue that would be produced in
the throw-away processes.  The Chemico-Basic magnesia F.G.D.
system was eventually selected by PEPCO and engineering for
the plant to be built at Dickerson Station commenced in
July 1971.  Construction of the plant started in July 1972
and was completed in August 1973.
     A limited test program had been planned for the PEPCO
operation as it was hoped that the major operating problems
would have been developed  and corrected in operation at the
first prototype in Boston by the time the Dickerson plant
was in operation.   However, a series of events including de-
layed start up of both the Boston Edison and the PEPCO pro-
ject, unanticipated problems found on starting up the processes,
and the lack of a regeneration facility for PEPCO's early
runs resulted in a restriction on the operation of the plant.
Those operations that were conducted evidenced areas requir-
ing additional, intensive investigation and development.
                      - 10 -

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 Some of these were:
     1)   Identification of the cause and remedy of
          agglomerates in the MgO slurry system.
     2)   Determination of losses and loss points as
          discrepancies in production and consumption
          calculations pointed to leaks of large mag-
          nitude in the magnesia system.
     3)   Determination of the extent and rate of cor-
          rosion as samples obtained from rail cars of
          MgSO3 shipped to Rumford showed much higher
          levels of iron contamination than any experienced
          in the Boston Edison Operation.
     4)   Establishing actual SO- and particle removal
          efficiencies.
     In order to provide information and solutions to these
problems, a more comprehensive development and test program
was prepared by Chemico and accepted by PEPCO in June 1974.
     A major factor in planning of the new program was the
extension of the data gathering and interpretation methods
that had  been used for the successful operations at Mystic
station to operations of Dickerson.  This immediately made
the large data and correlation file which had been developed
during the previous program accessible for extension and com-
parison with data generated from the coal fired application.
     The program was divided into a series of tasks and phases
in order to assure that the development proceeded in a fashion
that would establish priorities first,  attaining the funda-
mental requirements, and second leading to demonstration of
the system reliability,  if time permitted.
     The  first phase of the program was to determine control
parameters that would allow sustained plant operations under
conditions that established system equilibrium.  Complica-
                      - 11 -

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tions were encountered during this period because of
need to continue shake-down operations with new and modi-
fied equipment.
     The tasks slated for completion during this first
phase were:
     1)  Evaluation of changes to the MgO slurry
         system.
     2)  Determination of the complete material
         balance at the plant.
     3)  Measurement of system pH throughout the
         plant.
     4)  Preliminary measurements of SO, removal.
     5)  Preliminary operation with regenerated
         MgO from the calcining facility.
     6)  Evaluation of equilibrium conditions in
         the fly ash system with the precipitator
         in operation.
     7)  Coordination of operations during the pre-
         liminary system testing (conducted by an
         outside testing service) in order to pro-
         vide initial S02» SO., and particle control
         data.
     The second phase in the program had as its goal the
optimization of operation of the system at the Dickerson
site and determination of the process conditions at the
regeneration facility necessary to provide an alkali suit-
able for reuse after several cycles.  Some differences be-
tween the oil and coal fired applications could be expected
resulting from coal ash and/or first stage particle removal.
These differences would affect the:
     1)  Efficiency of SO- removal.
                     -  12  -

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     2)  Degree and rate of oxidation of the
         salts formed.
     3)  Efficiency of regeneration of MgO.
     4)  Activity of the regenerated MgO.
     Evaluation of these areas required an investigation
of the degree of contamination of MgO slurry with unre-
moved particulate matter and assessment of the S02 removal
efficiency of each stage for various cases.  This was to
be done concurrently with the determination of the effect
of fly ash contamination on the regenerated MgO and acid
plant in long term operations.
     In order to achieve these results in the shortest term
possible, extensive use was made of the data file complied
from the operating and analytical information logged during
the Boston Edison operations.  Using data processing methods,
conditions at the Dickerson plant could be quickly analyzed
and compared with information in the file.  In this way trends
indicating potential operating or process difficulties could
be rapidly identified and the necessary corrective action
taken so that maximum utilization of the intergrated plants
would be achieved.  The plan involved investigation of several
parameters, such as system pH, pressure drop, recycle and gas
flow and the resultant ash concentrations and solids levels
in the various streams, dryer temperature, and liquid flow
rates.
     Most variable excursions would occur as a natural effect
of process deviations.  With data recording, sampling and
chemical analysis on a routine schedule, they would be mea-
sured and their effects evaluated.  Some of the variables
such as gas flow and recycle  rates were  to  be artifically  varied
in order to reduce the danger of gross contamination of the
absorbent before the influence of the build-up of inerts on
                      -  13  -

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the process could be assessed.
     In order to determine the effect of changes in these
parameters a factorial experimental program was to be used
where possible.
     It can be anticipated that the widest excursions in
operating conditions would occur during the earliest part
of the program as the operators gain skill in running the
plant and as deliberate changes in conditions are made to
overcome process and mechanical problems.  As operations
continue, these variations diminish or disappear as greater
control is gained over the system so that steady conditions
will be experienced during the latter part of this period.
     Phase three of the program was to be a time extension
so that continuous operations under the optimized condi-
tions developed during Part II could be achieved.  The dura-
tion of this phase would be contingent upon the time required
to achieve three additional cycles of the inventory.  Over-
lap with the previous period would result in a total of five
regenerations of the magnesia and replacement of 1/2 of the
inventory.  This phase was never implemented.
Program Schedule
     Phase I of the program, the conclusion of the shake-
down operations and. the preliminary operational testing,
was estimated to require a one to two month period for com-
pletion.  System feasibility as well as the suitability of
the installed equipment was to be demonstrated in this
Phase I.  With this information plant design and equipment
selection could be undertaken for any similar installation.
     The second phase of the program, investigation of
varying operating conditions on performance for system
optimization and the determination of the quality of regener-
ated magnesia to obtain the required levels of SO- control
                      - 14 -

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was estimated to require an additional four months.  At
the conclusion of the testing program the detailed infor-
mation on operating values were to be used to fix control
parameters for the final phase.
     Phase three, a continuous operating period of three
to four months' duration was to conclude the program.
     A measure of the success of the program that was
achieved stems from the reorientation of the program from
the limited process guarantee tests to the more expansive
one described in the preceding sections.  In order to ac-
complish those goals, however, it was necessary to expand
the socpe of work that was being undertaken at the Dickerson
site.  Provision had to be made for a staff of chemists
and technicians to provide the analytical and testing sup-
port, technicians and operating engineers were necessary
to provide supervision and advisory services for the plant
operations and an overall organization had to be created
to direct the project, assimilate the data, implement the
changes necessary to solve the system problems and to co-
ordinate the operations being conducted at both Dickerson
and Rumford.
     This was accomplished through a joint agreement be-
tween PEPCO, Chemico and the Environmental Protection
Agency in which PEPCO provided the funding for the bulk of
the operations at both plants, Chemico provided the project
management function and EPA funded the analytical program
and its support.  EPA also provided funding for other
emissions testing programs conducted to determine the effect
of transient conditions.
                      -  15  -

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             3.0  PROCESS DESCRIPTION

     The pollution abatement system installed at PEPCO's
coal burning Dickerson Station on the Number 3 boiler is
composed of a particle control scrubber and an S02 control
absorber, both contained in a single, two stage unit
(Fig 1).  Particle control is effected by use of a Chemico
designed variable throat venturi as a first stage followed
by a venturi absorber using the Chemico-Basic Magnesium
Oxide System for Flue Gas Desulfurization (FGD) as the
second stage.  The particle control stage, including the
recycle and >slurry streams and fly ash thickening units
are independent and separate from the SO- control stage,
thus preventing fly ash contamination of the magnesia used
as the absorbent in that stage.  Both the particle control
streams and the F.G.D. streams are operated in a closed
loop mode.
     The original system concept was to provide a prototype
demonstration unit designed to process one-half of the flue
gas from the Unit 3 boiler, as shown in Fig. 2.  In one
configuration the flue gas to be treated is diverted from
the stack after the electrostatic precipitator by using the
venturi scrubber induced draft fan.  A second configuration
allows the ESP to be bypassed through new ductwork so that
tests could be conducted with the full particle loading
from the coal fired boiler treated in the wet scrubber unit.
In either case, the flue gas cleaned in the first stage
was processed for S0? removal in the second stage.
     In the Chemico-Basic process for sulfur dioxide removal
from flue gas the S02 is absorbed in a slurry containing
                     - 16 -

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FIGURE 1




   - 17 -

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       PR6.CIPITATOR
                      I.D.FAKJ   STACK
                          SCRUBBER
                                      SCROBBBg
                                        FAU
FGD  6AS PLOW SCHEMATIC
  DICKERSOKJ MC 3 " PEPCQ
       - 18  -

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magnesia, precipitating the solid magnesium sulfite.  The
magnesium sulfite, after appropriate steps to reduce its
moisture content, is then processed at a separate installa-
tion to regenerate the magnesia and recover the SO, for
use in chemical manufacture.  In this case the regenera-
tion was accomplished at the E.P.A. facility at Essex
Chemicals' Rumford Acid Plant in Rhode Island which had been
built for the New England S02 Control Project, with the
recovered S02 used in the manufacture of sulfuric acid.
3.0.1    Facility Description
      Dickerson Station is located on the Potomac River
outside the town of Dickerson, Maryland.  The plant is
situated in a rural, non industrialized area  about  35
miles northwest of Washington, D.C.  Coal is delivered
to the plant by rail.
      The station has three electric generators each rated
at 190 MW.  A fourth generator, rated at 800 MW is scheduled
for installation nearby on the plant site by 1982.  The in-
stalled 95 MW FGD system is sized to handle approximately
one-half the exhaust gas flow from Unit No. 3.  Pertinent
data on this Unit are given in Table 1.  Unit No. 3 has a
dry-bottom coal-fired boiler that was designed by Combustion
Engineering and installed in 1962.
      The coal presently burned has an average gross heating
value of 11,700 BTU/lb.  Average ash and sulfur contents
are 14 percent and 2 percent, respectively.
      The boiler is fitted with an electrostatic precipitator
(ESP) designed and installed by Research-Cottrell in 1962.
Particle collection efficiency was estimated to be 94 per-
cent.  The FGD system is installed so that it can receive
exhaust gas either from the outlet or breeching ahead of
the ESP.
                   - 19 -

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                    TABLE  1
 PERTINENT DATA ON PLANT DESIGN,  OPERATION
 	AND ATMOSPHERIC  EMISSIONS	

 Boiler data - Dickerson   No.  3  - PEPCO
 Rated Generating Capacity MW
 Average Capacity Factor  (1974),  %
 Boiler Manufacturer
 Year Placed In Service
 Unit Heat Rate, BTU/kwh
 Maximum Coal Consumption, Ton/Hr.
Maximum Heat Input, BTU/hr.
Stack Height Above Grade, Ft.
Flue Gas:  Design Rate, ACFM
           Maximum Rate, ACFM
Flue Gas Temperature, °F
Emission Controls:
     Particulate Matter
     so2

Particle Emission Rate:
     Allowable, g/scf dry
SO- Emission Rates:
     Allowable, Ib/Million BTU
 190
 81
 Combustion Engineering
 1962
 9180
 74.5
 1744 x  106
 400
 450,000
 650,000
 245
ESP with a venturi
scrubber on half
of gas flow.
Venturi absorber on
half of the gas flow.
 0.03
(1)
   1% sulfur coal equivalent
                       -  20 -

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3.0.2    Pollution Abatement System Description
     A schematic representation of the pollution abate-
ment process installed at the power plant is shown in
Fig. 3.  The principal element of the system is the two
stage venturi scrubber/absorber which combines in a single
vessel both particle removal and S0_ control.  Each of the
two functions are separated in the unit with the flue gas
being treated sequentially, first to remove fly ash then
to reduce its S02 content to acceptable levels.  Besides
providing the means of cleaning the flue gas, this sequence
assures that a negligible amount of fly ash will be cap-
tured in the magnesia slurry used for S02 removal in the
second stage.  This is necessary in order to prevent a
buildup of coal fly ash which would result in the contam-
ination of the regenerated MgO.  A further advantage of
this design is the ability to use the particle removal
stage independently should it be desirable to continue the
unit in operation without SC^ control.
     The Chemico/Basic1s Magnesium Oxide System for the
recovery of sulfur dioxide from plant flue gases utilizes
the sulfur dioxide absorption characteristics of an aqueous
slurry of magnesium sulfite, magnesium sulfate, and magnesium
oxide.   The process is accomplished in several steps:
                   Absorption
                   Dewatering & Drying
                   Materials Handling
                   Calcination
with the regeneration/recovery step (calcination) performed
at a remote site.
Absorption
     In the absorption step the process chemistry which
describes the removal of S02 from the flue gas can be most
                     -  21 -

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         THE DICKERSON REGENERATIVE WET SCRUBBING SYSTEM
                   POTOMAC ELECTRIC POWER CO. PROTOTYPE
                   PRECIPITATOR/SCRUBBER - ABSORBER
                MgO ADDITIVE SYSTEM FOR S02 RECOVERY
                           SCHEMATIC PROCESS FLOW SHEET
                                                          VENTURI
                                                       SCRUBBER/ABSORBER
                             1ST STAGE
                            ELECTRO-STATIC
                             PRECIPIIAIOI
                   TO DRY ASH HANDLING SYSTEM
                                                              OUST COUfCTOR
RECYCLED POND
  WATER
              TRANSFER
              TANK
CRYSTAL
ORYEI
                    M0O FROM ACID PLANT
          MgSOi 1O ACID
                                     Figure 3.

-------
simply explained as the diffusion of S02 through the flue
gas to a liquid surface, then absorption of the S02 with the
hydrated form of MgO, i.e.
      Mg°     + S0
         (aq)     2 -     3  (3-1)
The MgSO_ produced has a low solubility and can be separated
from the absorbing slurry as a solid.
      In the process, the flue gas containing sulfur oxides
enters a venturi absorber of special design, and contacts
the absorbing media which is an aqueous slurry of magnesium
oxide, magnesium sulfite, magnesium sulfate, and a small
percentage of other components.  The process of SO- removal
that occurs is explained by conventional mass transfer prin-
ciples.
      The venturi absorber can be considered as similar to
a co-current, packed vessel.  In the venturi the liquid
slurry is introduced and flows downward on a surface over
which passes an accelerating gas stream.  The high velocity gas
stream flowing over the liquid causes wave motion on the fluid
surface, the waves increase in amplitude and finally disperse
as fine droplets.  Thus, the whole mass of liquid can be dis-
tributed in the form of atomized droplets in the gas stream.
      There are several advantages in using the venturi as
an absorber.  The absorption surface is dispersed into and
flows with the gas stream during the time absorption is oc-
curing, thus eliminating the problems of plugging associated
with conventional packed towers (the surface area per unit
volume is approximately equivalent to dumped 3 inch rachig
rings) .  Due to system dynamics, this surface area relation
is relatively invariant over wide turn-down ratios, and high
removal efficiencies can be maintained over the normal operat-
ing range of the power plant's boiler.
                       -  23  -

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Dewatering  & Drying
      A stream from the absorption system enters a centri-
fuge where  the solids which were formed by the absorption
reaction in the slurry are separated.  This bleed stream
is controlled in order to maintain a constant solids con-
tent in the recycle slurry by removal of product magnesium
sulfite and unreacted magnesium oxide and any precipitated
magnesium sulfate.  The system is operated so that the ab-
sorbed S02  is removed as an equivalent amount of the mag-
nesium sulfur compounds.
      The wet centrifuge cake containing hydrated magnesium
sulfite, magnesium oxide and magnesium sulfate plus other
solids removed in the venturi absorber-centrifuge system
is passed to a rotary dryer to remove both unbound water
and most of the water of crystallization.  The dry product
is easy to  store, and the removal of water reduces shipping
costs.
Materials Handling
      The anhydrous magnesium sulfite and magnesium sulfate
produced in the dryer is conveyed to a storage silo for
transportation by rail or truck to the recovery acid plant.
The same transport is used to return regnerated magnesia to
the magnesium oxide silo at the power plant on the return
trip.
Calcination System
      Calcination is the process used for regeneration.  The
magnesium sulfite which has been separated and dried is
thermally decomposed as represented by the following reaction:
      MgS03	>MgO  +  S02   (3-2)
The recovered S02 is used in the production of sulfuric acid
and the regenerated MgO returned to the process for reuse.
The dry product transported to the regeneration acid plant
from the power plant is received, weighed and pneumatically
                       - 24 -

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conveyed to a storage silo.  It is fed to a direct-fired
rotary kiln at a metered rate, and calcined to both generate
sulfur dioxide gas and regenerate magnesium oxide.  Coke
can be added to provide a reducing atmosphere, as necessary,
to reduce the residual magnesium sulfate to the oxide and
sulfur dioxide.  The hot flue gas containing sulfur dioxide
and dust enters a cyclone where essentially all the dust is
removed and returned to the calciner.  The flue gas then en-
ters a venturi scrubber for final dust cleaning.  At the
same time, the gas is cooled and adiabatically saturated.
      The saturated flue gas is further cooled in a direct
contact packed tower to meet the requirements of the acid
plant water balance.  The cleaned flue gas then enters the
drying tower of an existing 50 T/D acid plant.  At the Essex
Chemicals' installation, the resultant product made from the
recovery of the sulfur dioxide is 98% sulfuric acid.
      The regenerated magnesia is cooled, conveyed to the
magnesia storage silo, and recycled back to the power plant.
3.1   DETAILED PROCESS DESCRIPTION
      The process flow sheet for the facility installed at
Dickerson is shown in Fig. 4, material balances are given in
Table 2 with the description of each item given in the Equip-
ment List, Table 3.
3.1.1     Particle Removal
      The first stage of the system uses a Chemico variable
throat venturi.  In this design, a 60° tapered plug is sus-
pended by a height adjustment mechanism in a 60° converging
section of the scrubber.  By stroking the mechanism through
its entire adjustment the throat opening can be varied allow-
ing up to a two foot maximum spacing.  In normal operation,
with standard liquor circulation rates, the throat width has
been adjusted to maintain an eleven inch pressure difference
across the particle removal stage.
                       -  25  -

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                                                                    VENTURI
                                                               5CRJBBIR/46SON6ER
                        \V STACE

                      UfCTRO-STATIC
                       PftfCIPlTATOR
                                                                     1A/ET     MIST
                                                                      FAN    ELIMINATOK

                                                                 TO Z* SI Aft*

                                                                          DUSTCOLLECTOR
                                    ICINTR4TC
                                   ^  TANK
TPAHSFIR

  TANK
CRYSTAL
 DRYIK
              FIOM 4CI6 PIAMT
                                     F I SURE A

                                P6PCO REGENERATIVE

                             WET SCRUBBING SYSTEM

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                                                            TABLE
                                              STREAM PROPERTIES ANO COMPOSITION
                                               SO2 AND FLY ASH REMOVAL SYSTEM
M
STREAM
NUMBERS
Temp.
Flow


•F
GPM
Solids Content.%
H2O
MgS03
MRSO«
MgSO3>6H2O
MgSO4.7H2O
MgO
Inert*
Fly Ash
Total
Fuel
STREAM
NUMBERS
Temp.
Pressure
Flow
S02
R2O
Dry Gas
Partlculate
Lb/Mln
Lb/Mln
Lb/Min
Lb/Mln
Lb/Mln
Lb/Min
Lb/Min
Lb/Mln
Lb/Mln
Btu/Hr

7

117
5.165
2.0
42. 870






875
43. 745

1
8

117
980
2.0
8.166






166
8.332

2
9


140
13.2
1.102






166
1.268

1
10
LIQUID AND

10.621
13.3
82. 850







95. 520

4
11
12 13 14 15 16
SOLID STREAMS

170
13.2
1.322


178
9.9
9.9
2.4
0
1.522

5
38.1
18.7

10.4 300
86.3
4.9
178 2.0
9.9
9.9 9.9 45.3 45.3
2.4 2.4 2.4 2.4
0 0
210.6 105.5 47.7 347.7
16.6x10*
6
GAS STREAMS
•F
In. W. G.
ACFM
Lb/Mln
Lb/Min
Lb/Mln
Lb/Mln
259
-11
295. 000
62.5
581
15.820
166.6
117
-26
263. 000
62.5
1.209
15.820
0.85
121
-36
286. 000
6.25
1.420
16.457
0.89
121
0
260. 000
6.25
1.420
16.457
0.89
450
-5.5
21.600



0.22
70
•0.6
10.200





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                      TABLE 3
EQUIPMENT LIST
                                                       Motor
                                                    Horsepower
Item Description
MgO Make-Up Tank
Dust Collector-MgO Silo
Thickener
Transfer Tank
Distribution Box
Sump Tank
Mother Liquor Tank
Dust Collector-Dryer
MgO Storage Silo
MgS03 Silo
MgO Feed Pump
First Stage Recycle Pump
Second Stage Recycle Pump
Underflow Pump
Transfer Pump
Sump Pump
Mother Liquor Pump
Induced Draft Fan
MgO Agitator
Mother Liquor Agitator
MgO Weigh Feeder
Dryer Feed Conveyor
Dryer Discharge Conveyor
Dryer Discharge Elevator
MgS03 Conveyor
MgSO, Weigh Feeder
Two-Stage Venturi Scrubber
Mist Eliminator
Variable Speed Coupling
Code No.
G-101
G-102
G-201 A,B
G-202
G-203
G-204
G-301
G-401
1-101
1-401
J-101 A,B
J-201 A,B
J-202 A,B,C
J-203 A,B,C,D
J-204 A,B
J-205
J-301 A,B
K-201
M-101
M-301
0-101
0-401
0-402
0-403
0-404
O-405
R-201
R-202
R-203
Quantity
1
1
2
1
1
1
1
1
1
1
2
2
3
4
2
1
2
1
1
1
1
1
1
1
1
1
1
1
1
(HP)










10
350
250

125
30
20
3500
5
3

1
2
2
2




                       -  28  -

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                      TABLE 3  (Cont'd)
EQUIPMENT LIST
                                                       Motor
                                                    Horsepower
                                                       if HP )  '
Item Description	Code No.    Quantity	v  '
Centrifuge                  R-301           1            200
Rotary Dryer                R-401           1            40
Dryer I.D. Fan              K-402           1            100
Instrument Air Dryer        V-101           1
                      - 29 -

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      Liquor is circulated in this particle removal stage
by recycle pumps, J-201 A & B (one operating, one spare,
each with a design capacity of 5700 GPM and driven by a
350 HP motor) through rubber lined distribution piping to
the upper level of the scrubber R-201.  The recycle flow
is split into two streams before reentering the scrubber.
The flow in each stream is adjusted and set by pinch valves
to provide uniform irrigation of the converging surfaces.
The outer converging section is supplied by ten 4" tangen-
tial nozzles while the adjustable cone is supplied by three
6" lines feeding a single bull nozzle.
      Flue gas enters the vessel and passes downwards through
the irrigated converging section.  As the gas is accelerated
through the throat the liquid film is atomized and distributed
through the gas stream.  Particle collection occurs on the
dispersed droplets through the mechanisms of impaction, dif-
fusion and attraction.  The flue gas and dispersed liquor
continue through the central down-comer to the basin area
of the first stage where the gas turns 180° upwards to pass
through the first stage mist eliminators.  The liquid drop-
lets are first disengaged in the turning zone and fall into
the first stage liquor pool, droplets small enough to be
carried with the gas stream are captured by the slot type
mist eliminator.  The cleaned gas continues out of the first
stage through the annular space between the outer shell and
the wall of the first stage reservoir.
      A bleed stream, about 15% of the total flow from the
recycle pumps, is sent to a distribution box and thence to
one of two thickeners, G-201 A & B, each of these is 40' in
diameter with a rake mechanism feeding a central underflow
discharge.  The thickened underflow, approximately 20 GPM
at 40 percent solids, is discharged to a distribution tank
where water from the lower pond is added and the mixture is
                       -  30  -

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pumped to the upper settling pond.  The pond overflow cas-
cades through a total of four settling ponds in series and
the clear water from the lowest is again returned to the
dilution tank.
      The thickener overflow drops into a transfer tank and
is returned to the first stage recycle loop by transfer
pumps J-204 A & B, (one operating, one spare, each designed
for 1190 GPM and driven by a 125 HP motor) so that closed
loop operation is maintained.
      It should be noted that the mechanisms for collection
of particulate matter or sulfur dioxide both depend on the
formation of droplets dispersed in the flowing gas.  In the
Chemico venturi the mechanism of atomizing the liquid by the
accelerated gas stream is the same for either stage.  How-
ever, the mode of operation of the stages is  different.
In the case of particle  collection a specific droplet size
distribution will be found to provide the maximum collection
efficiency and the size distribution is directly related to
a gas velocity flowing over the liquid surfaces.  In the
case of gas adsorption it is necessary to maintain a uniform
specific surface area (i.e. area of droplet surface per volume
of gas)  which in the venturi, is self regulating, after initial
adjustment, over a range of gas flows.  Thus, first stage
efficiency is maintained by operation at a fixed pressure
drop to keep the best droplet size distribution while second
stage efficiency is controlled by operation at fixed liquor
recycle rates to maintain a uniform surface area of the dis-
persed droplets.
3.1.2     Detailed Process Description - SO2 Removal
      In this system magnesia, both regenerated and make-up
material, is transferred from pneumatic discharge hopper
trucks to the elevated MgO storage bin through a 4 in.
pneumatic unloading system.  The MgO bin, 1-101, is 25 ft.
                       - 31 -

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in diameter and 46.5 ft high.  Magnesia is fed from the
silo, which is equipped with a vibrating hopper bottom,
0-103, to a 3760 gallon capacity MgO make-up tank G-101 by
an adjustable weigh feeder, 0-101, with mother liquor to
make the desired MgO slurry composition.  A small pre-mix
tank is interposed between the weighing system and the
steam heated make-up tank to insure dispersion of the MgO
powder and to act as a vapor seal.  Heated magnesia slurry
is added to the recycle stream by the MgO make-up pump,
J-101 A, B.  The magnesia slurry addition rate is controlled
by the operator to maintain the pH of the absorbing slurry
at the desired value.
      The recycle stream for the absorber is circulated at
a rate of 10,767 GPM by pumps, J-202 A, B and C,  (the capa-
city of each of these 250 HP pumps is half the design flow
of the recycle stream)  to provide a slurry dispersion within
the vessel sufficient for the desired S0~ removal.
      The recycle stream itself is split into two streams
for distribution before reentering the venturi absorber.
The flow in each stream is adjusted and set by plug valves
to provide a uniform irrigation to the converging surfaces.
Distribution of absorbing slurry is made by ten, six inch
tangential nozzles supplying the outer converging section
while the inner  cone is supplied by a single central nozzle.
      The slurry enters the upper part of the absorber stage
with the flue gas which is pulled through the system by the
I.D. fan K-201 driven by an 3500 HP motor, designed to handle
286,000 ACFM at a discharge head of -26 in. water.  The gas
and slurry mixture passes through the throat area into a di-
verging section, then into a central downcomer.  To exit the
vessel the flow of the cleaned flue gas turns one hundred
eighty degrees upwards.  In this step most of the larger
liquid droplets are disengaged from the flowing gas stream
and fall to the slurry pool in the conical base of the absor-
                       -  32  -

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ber.  The treated flue gas continues upwards through a slot-
type mist eliminator to further remove any entrained liquid
before the gas exits to wet fan K-201.  The fan wheel of
K-201, driven through a variable speed drive, is continuously
sprayed with water to prevent solids build up on the blades.
Entrained liquid in the gas stream leaving the fan is removed
in Mist Eliminator vessel R-202 before passing the stack.
      A stream of slurry, approximately 1.6% of the total
recycle, is taken from the discharge of the recycle pumps
to the centrifuge, R-301.  This is a 36 in. x 72 in. horizontal,
solid bowl unit driven by a 200 HP motor, and in normal
operations it removes 50% of the solids in the liquid stream
going to it.
      The solids separated in the centrifuge contain an
amount of SO- (as MgS03 or MgSO.) equivalent to the amount
removed in the absorber.  The centrate is discharged directly
to an agitated tank, G-301 of 1375 gallon capacity which
serves as a pump tank for this system, and then is returned
to the MgO slurrying system by pumps J-301 A & B.  The basin
of the absorber is the reservoir for the system and contains
approximately 20,000 gallons of slurry.  The other sources
of water entering the system are small amounts added as pump
seal water and an additional quantity used as a mist elimina-
tor wash; the latter is an intermittent addition.
      The centrifuge cake separated in the centrifuge is fed
to a dryer by screw conveyor O-401, a 35 ft. long unit with
a 12 in. diameter ribbon flight.  The dryer is a rotary unit
8 ft. in diameter by 50 ft. long.  Heat is supplied from an
integral 18 ft.  long oil fired combustion chamber at a maxi-
mum heat release rate of 26.3x10  BTU/hr.
      The dryer off-gas exits in to a cyclone, G-401, designed
for 97% removal of the solids entering with the gas.  From
the cyclone dust collector, the gas discharges via a booster
                      -  33 -

-------
fan, K-402, to the venturi absorber where, mixed with the
entering flue gas, it is cleaned of its remaining particle
load.  The separated fines collected by the cyclone returns
directly to the dry product pneumatic conveying system dis-
charging to the product silo.
      The dryer product is discharged to the dryer discharge
conveyor, D-402, 21.75 feet long unit with a 9 inch diameter
solid flight screw.  It then exits into a MgSO., weigh feeder
0-405 at the boot of the MgSO, discharge elevator, 0-403,
which is designed to handle 5 tons/hour of dried magnesium
sulfite.  The product then travels through another conveyor,
0-404, located on top of the MgS03 storage silo.  The stor-
age silo is 66.5 feet high and 25 feet in diameter, and is
equipped with a vibrating discharge hopper, 0-406.
      The product MgS03 is finally gravity loaded into a
waiting hopper truck for shipment to the MgO regeneration
plant.
3.2   DETAILED PROCESS DESCRIPTION - MAGNESIA REGENERATION
      SYSTEM
      Magnesium sulfite from the absorption system is received
at the regeneration facility. The regeneration section flow
sheet is shown  in Fig 5 .  Material balances are given in Table
4.  The salt is unloaded from hopper trucks to the sulfite
silo 1-401 through a 4 in. pneumatic conveying system similar
to that used for MgO at the power station.  The sulfite silo
was an existing tile structure, 25 ft. in diameter x 45 ft.
high, which was water-proofed before this use.  Sulfite is
unlaoded from this silo through a pair of inclined screw
conveyors, MgS03 conveyors 1 and 2, 0-509 and 0-510, equipped
with 12 in. diameter helicoid flights, which carry the
material from the below grade discharge spout to the boot
of the MgS03 elevator.
      This elevator,  O-511, a continuous discharge unit 54
ft. high,  is designed to handle 9 TPH of MgSO,.  It discharges
                      - 34 -

-------
ACIP

-------
                                                                TABLE 4-

                                                      STREAM PROPERTIES AND COMPOSITION
                                                           MgO REGENERATION SYSTEM
STREAM
NUMBERS
Temp °F
Pressure PSIG
Flow GPM
MgfHSO )2 Ib/Min
MgO Ib/Min
MgSO, Ib/Min
u
MgSO4 Ib/Min
Inerts Ib/Min
Fly Ash Ib/Min
Total Solids Ib/Min
H,O Ib/Min
Total Flow Ib/Min
Fuel Oil Ib/Min
STREAM
NUMBERS
Temp. ° F
Pressure In. W. C
Flow ACFM
Flow SCFM
Total Dry Gas Ib/Min
HJD Vapor Ib/Min
Total Wet Gas Ib/Min
SO Ib/Min
O, Ib/Min
Dry Gas MW
3 4 5 6 7 8 9 10 11 12 13





8.24
72.50
4.12
1.89
0.25
87.0

87.0

1









2

2

LIQUID & SOLID STREAMS
300



38.35


1.81
0.25
40.41

40.41

2
250

1.5









12
14
160

91








760

160 '

2
0.88


1.5
0.1

0.1
13.4
15.88

90

119








99.2

150

125.5








1045

150

80








65

Amb.

1.5








12

80

205








1708


GAS STREAMS
100
-45
2.980
2.460
206.2
9.0
215.2
44. 7
1.8
34.4
70
0
2.140
2.100
161




29
100
-45
640
529
39.0
0.8
39.8


29










U)
CTi

-------
to the MgS03 feed bin, G-506, a 6 ft. diameter by 11 ft.
high vessel equipped with a vibrating bottom, which also
serves as a surge bin for the weigh feeder 0-514.  This
weigh feeder is continuously variable to a maximum capacity
of 3.6 TPH and discharges to the calciner conveyor 0-512,
a 33 ft. long horizontal unit equipped with a 9 in. dia-
meter helicoid screw.  Coke is also discharged to this
screw which serves to mix the two components as calciner
feed prior to processing.
      The coke is pneumatically conveyed to the coke feed
bin G-505  9 ft. diameter x 19 ft. high, which also serves
as the storage bin for this material.  It is metered to the
calciner conveyor by a weigh feeder which is also continuously
variable up to a maximum capacity of 2.5 pounds per minute.
The two streams (3 and 4 of Fig.  5 ) enter at points 9 feet
apart and mix in the remaining 22 ft. section of the conveyor
before reaching the calciner elevator O-513, a 43 ft. high
centrifugal discharge unit.  This elevator feeds directly to
the calciner R-501.
      The calciner is a refractory lined, oil fired, rotary
kiln, 7 ft. 6 in.  ID and 120 ft. long.  Rotational speed is
variable between 1.5 and 2 RPM using a variable diameter
pulley drive, and the kiln has a slope of 3/8 in. per foot.
The calciner product empties into four tube coolers attached
to the shell and equipped with internal flights to contact
the existing hot regenerated magnesia with incoming air which
serves a secondary combustion air in the calciner, thus cool-
ing the calciner product before it empties to the MgO con-
veyor #1, 0-503.
      This is a 9 in. diameter helicoid screw conveyor,
54% ft. long, which elevates the product from the calciner
tube cooler discharge seventeen feet to an enclosure housing
the MgO processing equipment.  The regenerated MgO is dis-
                      - 37 -

-------
charged from 0-503 to a magnetic pulley for tramp iron
separation.  The MgO then passes through a 1 in. mesh
vibrating screen and enters a high speed pulverizer which
reduces it to the finished grind shown in Table 5.
      The cleaned, cooled, and pulverized regenerated mag-
nesia flows by gravity to the MgO elevator 0-504, a con-
tinuous discharge design, 89 ft. high, which brings the
material to the top of the MgO storage silo where it is
loaded by means of a horizontal screw conveyor  (MgO Con-
veyor #2) 0-505 equipped with a 9 in. helicoid screw.
      The MgO silo, 1-502, 25 ft. in diameter and 45 ft.
high is equipped with vibrating hopper bottom, 0-506, and
elevated on a structural steel support for direct gravity
loading of the returning trucks.
      The gas from the calciner, containing SO- and products
of combustion, as well as a small percentage of excess air,
is first partially cleaned of particles in the cyclone
dust collectors P-075.  This is a dual cyclone array, de-
signed for a 1 in. pressure drop.  The collected solids are
returned to the calciner with the feed to the unit.
      The partially cleaned calciner gas containing 8-10%
S02 is further cleaned in a venturi scrubber of Chemico's
special design, operated at a pressure drop of approximately
25 in. of H-O where it is also adiabatically saturated.  Next
the gas enters the separator tower section, which is an in-
tegral part of the venturi equipment.  The lower section of
this 4*s ft. diameter vessel serves a cyclonic liquid separa-
tor and the upper section, containing eight feet of 3*s in
pall rings is irrigated with cooled weak acid to further re-
duce the temperature of the gas to 100 F in order to main-
tain the acid plant's water balance.  A slip stream of cool-
ing liquor is stripped of dissolved SO- in the weak acid
                      - 38 -

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                TABLE 5

          DRY SCREEN ANALYSIS



Screen            Unpulverized             Pulverized
Size (Tyler)    Calciner Product       Calciner Product

+50                 30.3 %                    5.3 %

+100                18.1                      9.5


+200                 9.4                      8.8

+325                13.1                     49.8

-325                29.1                     26.6
                    -  39  -

-------
stripping tower P-502, a small  (15 in. diameter x  14  ft.
high) packed contactor.
      The stripped SO- joins the main gas stream and  is
ducted to the acid plant in 18  in. diameter, FRP pipe.
3.3   ACID PLANT
      The regeneration system was installed at the Rumford
acid plant of Essex Chemical Company located in Rumford,
RI.  The Rumford plant is located 55 miles from the instal-
lation at Mystic Station and haulage of the dryer and cal-
ciner products between these two sites was done by truck.
Both plants were equipped to load their respective products
from elevated silos and receive their feed by pneumatic un-
loading.
      The plant has been producing sulfuric acid since
1929 when it was built by Chemical Construction Corporation
and for the past several years all acid produced was  sold
in the merchant market  with no captive use.  Markets  for
the acid made at this plant are manufactured of detergents,
dyestuffs, Pharmaceuticals, aluminum sulfate,  tanning
chemical, steel pickling, boiler water treatment, lead-acid
batteries, galvanization, etc.  Sales in this market were
at the full published price, at the time of this program,
approximately $46 per ton  based on 100% H-SO,.  No change
in use or pricing was imposed when marketing the acid produced
from MgO regeneration.
      The plant is a contact sulfuric acid plant which uses
sulfur as raw material.  In the Chemico process the molten
sulfur is injected into the furnace using a spray burner,
with the process air first dried in a tower against 93% sul-
furic acid.  The catalyst is vanadium pentoxide.
      When first built in 1928 the Rumford plant was an in-
door plant typical of its time and had a capacity of about
                     - 40 -

-------
20 tons per day of 100% sulfuric acid.  Substantial
modifications were made to the plant in 1948 by Chemico
to increase its capacity to 50 tons per day.  The modifi-
cations included improved converters, a converter heat ex-
changer, waste heat boiler and economizer all installed out-
doors.  In addition, the cast iron cooling section was en-
larged and moved outside.
      This was the plant that was modified in 1971 to
accept the calciner off-gas essentially converting it to a
metallurgical  (roaster) gas plant; however, in the modifi-
cation the capability to continue to burn sulfur and aug-
ment the SOj from the regeneration plant was retained.
      Typical feed gas analyses to the acid unit are shown
in Table 6.

      The regeneration of magnesia, described in the pre-
vious section, produces an off-gas from the calciner approxi-
mately 100 fold richer in S0_ than the power plant combus-
tion gases treated in the S02 Absorption System.  The cal-
ciner gas is of sufficient strength to be used as a feed for
the manufacture of sulfuric acid.
      The small, sulfur burning acid plant (Fig. 6) required
some modifications to enable it to accept the calciner gas.
Provisions were also made during these modifications allow-
ing the plant to burn sulfur as an alternative source of
S02 or to operate on a combined feed from both combustion
of sulfur and gas from the regeneration plant.
3.3.1     Acid Plant Modifications
      The principal element replaced in the acid plant was
Main S02 Blower, K-901.  The original blower handled only
air required for the conversion of SO- to S03 and was not
designed to be gas tight (as required when feeding the acid
plant with gas containing SO-), or capable of the required
                      -  41 -

-------
                    TABLE 6
           SULFURIC ACID UNIT FEED GAS
              COMPOSITION/ MOLE %	
Source Of Gas          N2       cq2    q2     H20     S02

Regeneration Section   73        657       9

Sulfur Burning         79               12             9
                     - 42 -

-------
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   soa RJCM puoe
   a AS eflie I*
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*
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                             mneiM
                             •»(•
            *,
                         PUMP
                                 TO WES
                              CD-
                             93X PUMP
      L
                               X
                                                              TOW6.C
                                                                PRODUCT
                                         ORX
                                         TOWER
                                                    35t AGIO
                                                    •nraj
                                                             98^
                                                            a
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                                                                                              PRODUCT
                                                                                              TO
                                                                                           «-To
                                                                                            PUMP TANKS
                                                                                            • CM. R6TUBW
                                                                     TO ATMO&PM&Q&
                                                                             JS
                                                           IM1»1».         '"»•« M
                                                            iiia  1  i     fj alia I  •
                                                           ioono J—L    f^isaa^,!	1
                                                                        J?™,
                                                                    '. ACID TO STOBAQEl *
                                                                    MO PLOW
                                           98% PRODUCT
                                                 o sTon
                                                 / v
-------
control of suction pressure for operation of the re-
generation plant.  The replacement blower is an axial flow
compressor of 5,240 CFM capacity driven by a 200 HP motor.
It is capable of a suction pressure of up to 44 in. H-O for
the venturi pressure drop, duct and equipment losses, and
calciner draft at the regeneration plant, and a 75 in. H20
discharge pressure for the acid plant.  The unit was de-
signed to handle either air or a typical feed gas as shown
below:
                    ACID PLANT FEED GAS
                    S02             6.8%
                    02              9.4%
                    N2             74.7%
                    C02             8.1%
                    CO              0.9%
      The blower was equipped with an adjustable recycle
control in order to accommodate the variable feed rate of
the regeneration plant.
      Another important element added to the acid plant was
the Cold Heat Exchanger E-901.  This piece of equipment
supplies the heat to the incoming cold calciner gas equiva-
lent to that available in the gas when burning sulfur in the
sulfur furnace.  This is necessary to ensure that the gas
entering the first mass of the primary converter is hot
enough to sustain the reaction.  The exchanger, E-901, is
a vertical shell and tube unit 3 ft. diameter x 9 ft. high
containing 1700 sq. ft. of surface.  Hot gas exiting the
secondary converter enters the tube side on E-901 and heats
the calciner gas passing through the shell side to 540 F.
3.3.2     Acid Production
      In the acid plant, calciner gas enters (Stream 1 on
Fig.  6 )  and is diluted with sufficient air through the air
filter for conversion and passes to the acid plant's drying
                     - 44 -

-------
tower where it is contacted with 93% sulfuric acid to re-
move the water from the gas.  Entrained liquid is removed
in F-901A, the Dry Tower.  Any S02 absorbed by the 93% acid
is stripped in the new Tower (F-903), a 30 in.  diameter x 15 ft. high
ceramic tower containing a 10 ft. bed of 1% in.  saddles,
and returned to the main gas stream.  The small amount of
additional air is used for trim of the oxygen concentration.
The gas is pressurized by the S02 blower and enters  the  Cold
Heat Exchanger, passes to the Converter Heat Exchanger,  E-902
and finally enters the converters H-901 A  & B.  The  heat
balance for the conversion step is maintained by using  the
gas from the second mass of the Primary Converter, H-901A,
to heat the gas from the Cold Exchanger, and the gas leaving
the fourth mass of the secondary converter, to heat  the
incoming feed.
      Next, the stream containing 6.7% SO., is contacted  with
98% H2S04 in the Absorption Tower F-902 A  & B.  The  gas
streams from these towers are first demisted in R-902 A  & B,
then the remaining SO- is removed in the Tail Gas Scrubbing
section shown in Fig. 7 and Table 7 to reduce the concentra-
tion of S02 leaving the plant to allowable levels.
      The absorbant used in the Tail Gas Scrubbing section
is NaOH solution.
      In order to allow a rapid change to  sulfur burning,
when the plant is operated on 100% calciner gas, the sulfur
furnace was equipped for oil firing.  The  combustion products
from this operation are vented to the atmosphere through a
short stack which could be bypassed.  In normal operation,
however, sulfur was burned concurrently because of a low
MgS03 feed rate.  This procedure had the advantage of allow-
ing a rapid change should the calciner gas flow be interrupted.
This alternative was possible because of the several dampers
which had been incorporated in the ductwork.
                      - 45 -

-------
     , WATtK
     CE. TA,
     FSZOKA
OM A BATCH
                                                                          TO
                                                                           NU!
                                                                         PJMP
—BECVCUE
 -RjfAP
— J-107.
                PKS.URE 7

      TAIL GAS.  SCRUBBING SYSTEM

-------
           TABLE 1
STREAM PROPERTIES AND COMPOSITION

    TAIL GAS SCRUBBER SYSTEM
STREAM NUMBERS
Temperature ° F
Pressure IN WC
Flow ACFM

Dry Gas Ih/Min
H2O Ih/Min
Wet Gas Ib/Min
SO2 (Design) Ih/Min
^ SO2 PPM Dry
•"• By Volume
1
160
0
4,250

279
0
279
3.0
5000

2
165
14
4140

279
0
279
3.0
5000

3
77
0
5600

276.3
5.6
281.9
0.3
500

STREAM NUMBERS
Temperature ' F
Flow GPM

NaOll Ib/Min
Na -SO, Ih/Mm
i 3

H2O Liquid Ib/Min
Total Solution Ib/Min

4 5 678
77
152


299


1266
1565

Amb.
0.6

3.75



3.75
7.5

77
3.0


5.9


23.6
29.5

Amb.
3.0





24.6
24.6

77
76*


149. 5


133
782.5


-------
    4.0  POLLUTION ABATEMENT SYSTEM PERFORMANCE

    Construction and check out of the system at Dickerson was
completed by September of 1973 and gas was first passed to
the unit on September 14th.  In the following three month
period 600 hours of operation were logged in the initial
operation and debugging of the system.  Most operating periods
were of short duration, from 10 to 24 hours, before a system
problem would force a halt.  The major problem area encountered
in the earliest runs was the MgO feed system, where plugging
occurred in both the mix tank and slurry lines.  The plugging
was partially remedied by two modifications: the installation
of a premix tank before the slaking tank to assure complete
wetting of the MgO powder with recycle liquor, and addition of
a steam sparging system to the tank.  Both these remedies
have also been found necessary to correct similar problems in
the oil-fired application.
    Other shut-downs in this period were caused by leaks that
developed in the venturi scrubber internal piping between first
and second stages.  The leaks occurred in expansion joints
where sections of the recycle lines left the first stage re-
servoir.  Testing showed the joints supplied were off-specifi-
cation stainless steel that was not resistant to this acidic
stream.
    Despite these problems two sequential six-day runs inter-
rupted by a 24 hour boiler outage, were attained in the pre-
liminary operations.  While these runs did  show the operability
of the entire system their usefulness in assessing chemical
stability was limited because of high entrainment losses from
the venturi which prevented equilibrium conditions from being
attained in the recycle streams.  A low S0_ removal efficiency
was also noted in the preliminary testing.

                     - 48 -

-------
    An inspection of the scrubber in January 1974 showed
that off-specification material, unresistant to the acidic
environment of the first stage, had also been used in bolts,
nuts, hanger rods, spray nozzles and some piping in the
vessel.  A major shut-down extending over the next six months
was taken to replace corroded parts and repair damaged
areas.  A policy was also adopted to test each replacement
item to ensure that it was of the specified type 316 stain-
less steel.  A brief verification run was made at the be-
ginning of May and the new problems which it uncovered were
corrected in the following weeks, prior to starting regular
operations.
    During this initial operating period MgO regeneration
was not available to the Dickerson plant.  The EPA unit
located at Rumford, Rhode Island was being used exclusively
for regeneration of the MgO from the oil-fired system proto-
type.  The regeneration plant was not scheduled to be avail-
able for Dickerson Station till July 1, 1974, when PEPCO
would then have exclusive use of the facility.  In antici-
pation of this use, PEPCO sent three rail cars of MgS03 from
its operations to the Rumford facility for preliminary testing
of magnesium sulfite derived from coal fired operation.
    Before operations with regenerated MgO were started at
the power plant some additional test work was conducted in
June 1974.  The low S02 removal efficiency, first noted in
the debugging runs, was confirmed by these test runs and
attributed to a low (1" to 3"^^P) second stage pressure drop.
A restrictor, to reduce the second stage throat area by 40%,
was designed in order to increase the pressure drop to design
value.
    The test runs exhausted the initial supply of MgO which
had been delivered for start up operations.  The abatement
                     - 49 -

-------
system was idle for another six week period, awaiting a
new shipment of MgO, the return of regenerated magnesia
from Rhode Island and installation of the throat restric-
tor.
4.1  DEVELOPMENT TEST PROGRAM
     The silos at the regeneration plant were completely
emptied of all Boston Edison MgSO3 in July 1974 and  filled
with  PEPCO material from the  rail  cars.   (The
lack of any size reduction or lump breaking equipment in
the path between the Dickerson dryer and regeneration
plant calciner caused unloading problems then,  and through-
out the entire program).  The operation, after a brief one-
day adjustment period, produced a calciner product which
tests showed to be of acceptable quality for recycle.
     When the PEPCO MgSO^ was processed in the calcining
facility, it was found necessary to add carbon to the feed
to effect the reduction of magnesium sulfate.  The oil de-
rived calciner feed had contained sufficient carbon to satisfy
the reduction reaction needs as the absorber, in the oil-fired
application,  treated the gas directly from the boiler.  This
"scrubbed" out the soot and uncombusted fuel associated with
oil-fired applications which not only reduced the power
plants particle emissions but also provided the 0.5 to 1%
carbon required in the process for reduction of MgSO..
     Because of the necessity to prevent fly ash contamina-
tion of the recycled magnesia in the coal-fired application,
the incoming flue gas at PEPCO was precleaned (by ESP and/or
scrubber) to remove the fly ash.  This also removed any car-
bon sources from the flue gas before it entered the second
stage.
                  - 50 -

-------
    A supply of petroleum coke was located and added in
the required proportions with the calciner feed.  This
was continued throughout the integrated operations at the
acid plant with Dickerson Station.
    These initial operations at the regeneration plant also
saw the return of the "slide" problem which had been en-
countered and partially solved for the oil-fired application.
(A "slide" was a description of a rapid emptying of a part
of the calciner charge before decomposition of all the MgS03
in it).  The slides caused overloading of the materials
handling equipment on the kiln discharge, when they occurred,
which forced a reduction in the kiln feed rate.  Analysis of
the product after a slide showed several percent of undecom-
posed MgS03.  The frequency of occurrence of slides was
eventually related to the size distribution of the entering
feed.  It was shown that a high percentage of fines in the
feed triggered them.  By adjusting the methods of operation
of the dryer to reduce the amount of fines in the dried MgSO^
during the oil-fired application calciner feed rates up to
80 Ib/min were able to be achieved.
    A different type dryer than the one used in the oil-fired
boiler application had been designed for the PEPCO operation.
(A counter-current design dryer had been installed at Boston
Edison Company's Mystic Station while a co-current design
dryer was installed at Dickerson Station).  This difference
in dryer types was one of the major equipment differences be-
tween the oil-fired boiler and coal-fired boiler applications
in the MgO slurry dewatering process.
    Analysis of the product from the PEPCO dryer showed that a
higher percentage of fines were produced from the co-current
dryer and that the fines could not be controlled by the tech-
                     - 51 -

-------
niques used at Mystic Station.  The slide problem limited
calciner feed rates to 40 Ib/min rather than the 106 Ib/min
design rate.  Because of the interrupted operations of the
plant a dryer investigation could not be undertaken during
the program, and calciner feed rates were held at 40 Ib/min.
However, this rate was sufficient to keep the FGD operation
supplied with recycle MgO.
    At Dickerson Station a shipment of virgin MgO was received
July 29th and the first regenerated MgO was returned August
16th.  With this inventory of material the performance test-
ing phase was started to provide preliminary reliability data
and optimization information.
    Tests conducted over the following two weeks checked SO-
removal efficiency prior to installation of the throat re-
strictor and tested a new configuration for MgO pre-mixing
using an eductor mixer.   (The mixing test was inconclusive
because the unit obtained was too small and plugged).  The
MgO slurrying system was returned to the original configura-
tion, an agitated pre-mix tank.  The throat restrictor was
also installed in preparation for the series of performance
tests which were to follow.
    The first six series of performance tests were started during
the last week of August and the test program continued through
the months of September with 400 hours of operation logged.
Test series conditions included full to half boiler load
with full to half design flow to the scrubber/absorber, and
inlet gas taken after the precipitators or with no pre-clean-
ing.  Series designations are shown in Tables .  A descrip-
tion of these tests and the results are presented in another
section of this report.  Also incorporated into the foregoing
investigation was an analysis program of the first stage re-
cycle liquor, thickener and pond and river discharge flows
                     - 52 -

-------
                  TABLE  8

       PERFORMANCE TEST DESIGNATIONS
Test
Series
   Boiler
    Load
(%  of  Design)
  Scrubber
     Gas
(% of Design)
Scrubbed Gas
  Pretreated
5A
5B
6
7
8
100
50
100
100
100
100
50
50
100
50
E.S.P
E.S.P
E.S.P
NONE
NONE
                     - 53 -

-------
for a number of chemical species of environmental signifi-
cance.
    Following these tests the plant was readied for the
balance of the optimization program.  Emphasis was placed
on the assessment of the effect of coal fly ash on the re-
generation and utilization of the recycled magnesia.  A
regular sampling and analysis program was initiated for flue
gas monitoring and chemical determination of all major stream
compositions.  Over the next four months, system operations
totaling 1350 hours provided much information on the effect
of regeneration operations on the absorption of sulfur dioxide/
operation of the centrifuge and dryer and the conditions of
scrubber/absorber operation.
    Attainment of the major goals of the project, multiple
recycles of magnesia and conclusive demonstration of system
reliability were thwarted by the deteriorated condition of
the piping which evidenced itself almost immediately after
entering this phase of the demonstration program.  As the
performance testing was completed the first of many failures
in the rubber lined, first stage recycle piping occurred
forcing a shut-down of the system.  During the rest of the
operations first and second stage pipe failure was the most
common shut-down cause.  A summary of operations during this
period is given in Table 9.
    Some improvements were obtained when several sections
of the second stage recycle pipe were replaced but leaks
in the other sections and the unrectified first stage problem
limited operating periods to days rather than weeks.  The
longest continuous run during this period was eleven days
from December 13th through December 23rd.  Operations re-
sumed on December 27th and continued into January 1975 with
tests of first stage operation alone.  These tests also
                     - 54 -

-------
                                  TABLE 9

                     SUMMARY OF OPERATIONS FGD SYSTEM
                        PERFORMANCE TEST PHASE
Week Ending
11/01
1V08
11/15
11/22
11/29
12/06
12/13
12/20
12/27
01/03
01/10
01/17
01/24
01/31
Goal
System Repair
Repair
Operate at design load
Establish dependable &
continuous operation
Continuous Operation
Continuous Operation
Continuous Operation
Continuous Operation
Continuous Operation
Continuous Operation
Operate 1st Stage only
Continuous Operation
Continuous Operation
Continous Operation
Problem Areas


Centrate Punp
Bucket Elevator (1)
& Piping Leaks
Dryer Fan Drive
Piping Leaks
Piping Leaks &
valve failure
Piping Leaks
Piping leaks &
valve failure
Piping leaks

MgO inventory
depleted
Piping Leaks &
Conveyor Jam
Piping Leaks
Number Of
Interruptions

1
2
1
1
2
1
2
1

1
1
1
Avg.
Load


60-80%
60-70%
70-80%
75-80%
60-80%
60-85%
60-90%
80-90%
90-100%
60-70%
50-60%
50-60%
Hours Of
Operation
0
0
88
84
123
77%
114%
159%
83%
53
78
75
30
37%
1003.5
1)   Marginal bucket elevator capacity limited operation
    to average 70% of design
                                                            OVERALL AVAILABILITY 46.1%

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provided data on first stage SO, removal capacity.  A
final series tested recycle liquor flow effect on S02 re-
moval efficiency.
     Operation of the regeneration plant during this period
was sporadic because of the outages at Dickerson and the
resultant interruptions in feed to be calcined.  The major
mechanical problem encountered at the regeneration plant
was a failure of the pinion gear in the main drive on the
calciner (due to misalignment and lack of lubrication).   A
replacement was locally fabricated and the unit was only
out of service for two weeks during December.  A summary
of operations at the regeneration facilities is given in
Table 10.
     During the program approximately 2247 tons of MgSO~
were processed to MgO at the acid plant.
     During January 1975 plans were made for major over-
haul of the PEPCO FGD system including replacement of all
"thin" second stage pipe and repair of several sections-of
first stage rubber lined pipe.  This work was scheduled in
conjunction with PEPCO1s planned 12 week overhaul of its
No. 3 boiler and turbine.  Repair of the FGD system was
for the most part, completed by April.  PEPCO, however,  dis-
covered a major defect in the No. 3 turbine during their
boiler overhaul which necessitated a number of extensions
of their boiler outage.  Eventually the outage extended to
the end of July 1975.  The outage extensions created
secondary problems in the financing of the project and the
program was terminated.
                  - 56 -

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                       TABLE 10
        SUMMARY OF OPERATIONS CALdNER SYSTEM
              PERFORMANCE TEST PHASE
Week Ending

11/01/74
11/08/74
11/15/74
11/22/74

11/29/74
12/06/74
12/13/74
12/20/74

12/27/74

01/10/75

01/17/75
01/24/75
01/31/75
Maintenance on Bucket Elevator
Routine Maintenance
Routine Maintenance - Accumulate MgS03 Inventory
Routine Maintenance - Accumulate MgSO3 Inventory
      START-UP
MgO Production for PEPCO
MgO Production for PEPCO
MgO Production for PEPCO
Maintenance on Calciner Main Drive and MgO
  Production for PEPCO
Complete Repairs on Calciner Main Drive and MgO
  Production for PEOCO
Run Test on Boston Edison MgSO, without Coke
    Addition
Test PEPCO MgSO3 without Coke Addition
MgO Production for PEPCO
MgO Production for PEPCO
Operated For
   Hours

     0
     0
     0
     58
     47
     87.4
     24
      8.9
    100.9

     44.2
      4.5
      7.9
                         -  57 -

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4.1.1  October 1974 - Details
      Regular operation of the FGD system at Dickerson was
resumed after the performance test work on September 30.
This first operation was stopped after three days when pro-
blems with the MgO premix tank forced an outage.  The sys-
tem was restarted at 1 p.m. on the 3rd and ran continuously
for the next 12 days at approximately 50 to 80% of design
load.  A failure of a 14" rubber lined pipe elbow in the
first stage recycle loop forced another outage at 4 p.m. on
the 14th.
      The analytical program was fully implemented by October
16, 1974.  The scrubber ran from a start up at 12:00 a.m.,
October 16 to 9:00 a.m., October 18.  A planned shutdown was
taken to repair several leaks in the first stage recycle
lines and to attempt to increase the flows in MgO slurry feed
system.  The scheduled repair was completed by noon, October
18, however, after operations resumed low flow of MgO slurry
resulted in loss of pH control in the second stage.  Leaks
in the MgO magnetic flow meters also caused delays.  Flue
gas treatment resumed at 3 a.m. October 23, 1974.
      During the night of the 24th problems again occurred
in the MgO slurry system with line plugging reducing pH in
the second stage to 6.6; however, the situation was corrected
and the system ran till 9 a.m. on the 25th when the unit was
shut down for a boiler tube leak.  The boiler was repaired
by October 28,  but the scrubber system was waiting for main-
tenance and was not returned to service.
4.1.2  November 1974 - Details
      During the 30 day period, November 1 to November 30,
1974, the scrubber operated 318.9 hours out of a possible
720 hours for a 44.3% availability.  During the period of
operation the unit ran at 50% to 100% of design gas load
                     - 58 -

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resulting in a total average available capacity for the
month of November of 34%.  Because of scheduled outage
in the earlier portion of the month for leak repair and
overall maintenance, most running time was logged in the
latter portion of the month.
Scrubber Operation and Comments
      The scrubber was brought on-line at 2 a.m., November
10, at 80% of design flow.  Attempts to increase the gas
flow to full load were hindered, as problems in the MgO-
slurry feed system prevented pH control at increased loads.
The system operated steadily, adjusting the scrubber gas
flow to maintain a pH of 5.7, till 2:20 a.m. on the llth,
when the scrubber was taken off-line due to a leak at the
inlet of the second stage bleed line.
      Repairs were completed at 8:00 p.m. on the 13th.
The system was returned to operation and the scrubber load
was varied between 60 and 80% to compensate for station
load changes during this period.  On November 15, at 10 a.m.,
a reduction to 1/2 load was made to repair a leak in the
centrifuge.  When the centrifuge was diverted, the solids
in the second stage recycle slurry reached a high level
and the low load was maintained until the solids level was
centrifuged down.  At this time it was noted that the flow
to the centrifuge had dropped to 55 gallons per minute,
which prevented operating the unit at design gas loading.
This was corrected by operating with both the main and
spare pump.  The plant continued in operation with the
scrubber load gradually increased to 100%., holding pH in
the 7.0 to 7.3 range.  (Normal operating practice was to
control pH by maintaining a steady MgO feed, adjusting the
gas flow to maintain the pH set point affected by variations
in the coals sulfur content).
                      -  59  -

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      A leak developed in a first stage recycle control
valve and the unit was taken off the line to make repairs
on the 16th.  Operations resumed on the 19th and continued
through the 21st when the belt drive failed on the dryer
I.D. fan.
      The fan repairs were completed and gas was put back
into the scrubber at 3:15 p.m. on November 23, but by 11 p.m.
the No. 3 boiler developed a tube leak, forcing a shutdown.
This was repaired and operations resumed by 2:40 a.m. on the
24th, six hours later another interruption was needed to re-
pair a bearing on the dryer product screw conveyor.  The
system was returned to operation 2:45 that afternoon and
operated continuously through the end of the month.  Operat-
ing adjustment had to be made during this period to accommo-
date generating station coal feeder problems.
      During this final fifteen day period the scrubber
operated a total of 241.6 hours out of a possible 360 hours
for a 67.1% availability (51.7% average available capacity
based on a 77% of design gas flow).
4.1.3  December 1974 - Details
      During the 31 day period, December 1, 1974 to
December 31, 1974, the scrubber operated 430.8 hours of a
possible 744 hours, an availability of 57.9%.
      During the month of December various new studies were
initiated and the wet chemical method for the specific deter-
mination of MgS03.6H20 and MgS03.3H20 in the mixture was
used to determine the hydrate ratio in the centrifuge cake
samples.  Previously, the ratio of MgSO.,. 6H20/MgSO_ .3H_0
had been approximately determined on the basis of percent
combined water (water of crystallization) as determined on an
OHAUS moisture balance.
      Chloride in the system was also measured as a function
of operating time.


                     - 60 -

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Scrubber/Absorber Operation and Comments
      The run which had started on November  24 had to be
aborted on December 1 after a leak developed in  the rubber-
lined bleed line to the thickener area.  Operations were
again resumed on December 5 and continued till 4:30 a.m.
on the llth when leaks in the first stage bleed  line again
forced an outage.  During this period adjustments in operat-
ing conditions were used to control problems of  MgO feed,
station coal handling and centrifuge cake buildup in the
discharge hopper.
      Operations were resumed at 6 p.m. on the 13th and
this run continued till the 23rd when leaks  in both the
first and second stage discharge headers forced  a shutdown.
      The system was restarted on the 27th but the run was
aborted on the 29th after 64 hours of operation  with another
recycle pipe failure.
4.1.4  January 1975 - Details
      Measurements of the pipe wall thickness and observa-
tions of the pipe involved in the  numerous   failures which
had been encountered showed that a major system  overhaul and
pipe replacement program was necessary if any'sustained
operations were to be achieved.  PEPCO has rescheduled an
overhaul of the No. 3 generating unit to 1975.   This was a
five year inspection and overhaul of the generator originally
due in 1973.  Plans were made to recondition the scrubber
system during the boiler outage scheduled to start in January 1975.
Some additional test work was conducted with the pollution
abatement system during January while waiting for the  planned
boiler shutdown.
      These tests included four days of operation with first
stage (particle control) only, and another series of tests
to determine the effect of variation of recycle  flow rate on
SO- removal efficiency.
                     - 61 -

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4.2  UTILITIES CONSUMPTION
     Electric power consumption  (in MW/Day) of the particle
control and flue gas desulfurization system installed at
Dickerson Station is given in Table 11 for the major operat-
ing periods of the test program.
     Also included in the table are data on average fuel
consumption for the dryer used in the FGD system along with
an approximate gas flow processed during the period.  While
there is some effect caused by the variation in fuel sulfur
content on the amount of centrifuge cake produced it appears
that a significant factor in dryer fuel oil consumption is
the weather.  Fuel consumption is seen to increase during
the winter months and decrease during the summer months
while the gas flow processed through the system remained the
same.
4.3  MgO CONSUMPTION
     Magnesia consumption during the fifteen month period
of operation of the plant was high.  It is evident that the
loss rate during the period of initial operations was higher
than the loss rate during the latter planned operations
phase.
     MgO shipments to the plant were made corresponding to
these two periods.  An initial inventory of 357 tons of
MgO was shipped to Dickerson between August and December
of 1973 for the start-up operation.  An additional 281.3
tons of virgin magnesia wereadded as make-up between July
and November 1974 for the planned operations phase.  The
addition of make-up MgO at Dickerson between July and
November is given in Table 12.
                     - 62 -

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       TABLE 11
UTILITIES CONSUMPTION
     FGD SYSTEM

Major
Operating
Periods
April 25-30, 1974
June 13-16, 1974
Aug. 13-17, 1974
Sept. 3-11, 1974
Oct. 16-18, 1974
Nov. 24 - Dec. 1, 1974
Dec. 6-10, 1974
Dec. 14-23, 1974
Dec. 27-29, 1974
Jan. 12-14, 1975
Aug. 12-14, 1975
Aug. 22-26, 1975

Approximate
Gas Flow
% of Design




66%
75%
70%
67%
80%
70%
70%

Average
Electric Power
Consumption
MWH/Day
38.6
39.8
34.8
27.7
41.8
53.3
49.0
45.5
57.5
50.0
50.0
33.8
Average
Dryer Fuel
Consumption
GPM
0.57
0.39
0.33
0.38
0.72
0.93
0.95
0.91
0.96
0.93
0.54
0.32
          - 63 -

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                  TABLE 12
                MgO MAKE UP
                FGD SYSTEM
Date

7/29/74

9/1/74

10/24/74

11/4/74
Quantity Of Virgin
   MgO Received

     67.6 Tons

     73.4 Tons

     67.4 Tons

     72.9 Tons
    281.3 Tons
                     - 64 -

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4.3.1  Losses - Preliminary Operations
     Estimation of dryer product generated at Dickerson
Station based on shipping records showed 485 tons of MgSO-
were produced from the initial charge of 357 tons of MgO.
This accounts for only 55% of the dryer product that should
have been produced based on the design material balance.
    An inventory evaluation also showed that 144 tons of
MgO equivalent were lost during the same period giving a
loss rate of 40.4% of the material fed.  Since no magnesia
regeneration was being performed during the early period
the losses were essentially confined to the FGD system
site.  Part of the loss can be attributed to a number of
unmeasured spills anddischarges   during this period, some
of these were:
    1)  Material discarded when cleaning out the MgO
        slurry system after a plug.
    2)  Material lost when draining the scrubber for
        repair work.
    3)  Spills of dryer product due to material handling
        equipment overloads.
     Another major loss point was entrainment and overflow
from the second stage of the scrubber.  The few chemical
analyses of recirculating  slurry taken during the early
period showed a maximum of 8% magnesium sulfate in this
stream.  Since a concentration of 15% to 18% MgSO. is ex-
pected in the equilibrium system the low concentration in-
dicated a  large  bleed  (or  leak)  from the  magnesia  recycle
loop.
    Chemical analysis of the fan sump discharge during the
performance testing conducted in August and September 1974
showed high levels of magnesium salts and solids in this
stream.  Analysis showed MgS04 concentrations as high as
                     - 65 -

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 10%  again indicative of excessive  entrainment.   The
 entrainment was probably the  major loss  point sustained
 during these preliminary operations.
 4.3.2   Losses - Planned Operational Testing Period
     Corrective action was taken to reduce  the entrainment
 from the scrubber system by lowering the operating  liquid
 level  in the second stage reservoir from 80% to  40% to  re-
 duce gas velocity in that zone.  Analysis  of the fan sump
 pit  discharge in early October  1973 showed much  lower MgS04
 concentration.   Losses from this source  were reduced to less
 than 0.5% (based on Mg   content of the  fan discharge)  during
 the  final three months.
 4.4  MgO REGENERATION
     MgO inventory recording was started  at Dickerson in
 October 1974 and the weekly inventory records are summarized
 for  the period of operation in  Tables 13  and 14 .
     Test work at Dickerson in August had been carried out
 using  regenerated MgO;  however,  the losses,  which had occurred
 before the development program  was initiated,  necessitated re-
plenishment of the inventory with virgin  MgO.  During September
 and  October 141 tons of MgO were received  and 109 tons  of re-
 generated alkali were returned  from Rumford for  operation of
 the  integrated system.   During  October the Dickerson system
 operated 420 hours of a possible 647  hours, consuming 80% of
 the  alkali available and producing 482 tons of dryer product.
     Thus,  at the start of November, 141.4  tons of MgO and
 100.6  tons of MgS03 were on hand at Dickerson.   Of  the  MgO,
 approximately 65% had been regenerated at  least  twice.   Be-
 fore operations were resumed  at Dickerson  73 additional tqns
 of virgin MgO was received and  added  to  the silo.   Inventory
 on November 8th,  for the resumption of Phase II  of  the  de-
 velopment program,  was 213.3  tons  of  MgO and 100.6  tons of
                     - 66 -

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              TABLE 13
INVENTORY SUMMARY BY WEEK-FGD SYSTEM
Week Ending
11/1/74
11/8/74
11/15/74
11/22/74
11/29/74
12/6/74
12/13/74
12/20/74
12/27/74
1/3/75
1/10/75
1/17/75
1/24/75
1/31/75
MgS03
Produced
0
0
32.8
98.4
142.5
54.0
116.8
157.9
83.6
65.0
0
85.9
8.0
	
(Tons)
Shipped
19.5
0
20.9
35.4
141.2
141.4
35.1
108.6
114.6
0
0
88.5
76.3
43.2
824.7
Closing^
MgO
110.4
182.3
150.5
105.2
110.1
131.0
68.2
26.9
73.9
48.9
48.9
54.8
118.3
105.1
(Tons)
MgSO
56.6
56.5
68.4
131.4
123.3
14.0
95.9
145.1
96.2
161.2
161.2
158.5
90.2
71.5

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                      TABLE 14
INVENTORY SUMMARY BY WEEK-REGENERATION SYSTEM
Week Ending
11/1/74
11/8/74
11/15/73
11/22/74
11/24/74
1 12/6/74
£ 12/13/74
1 12/20/74
12/27/74
1/3/75
1/10/75
1/17/75
1/24/75
1/31/75
MgO
Produced
0
0
0
30
26.4
50.3
13.3
4.9
0
48.2
56.5
30.6
2.5
4.4
(Tons)
Shipped
11.9
0
0
0
91.7
35.5
27.8
15.7
0
12.8
0
53.8
71.0
0
Closing
MgO
31
31
31
61
11.5
26.3
11.8
0
0
35.4
90.9
67.7
1.5
5.9
(Tons)
MgSO3
44
44
44
8
45.1
52.6
62.1
156
233.4
126.4
0
7.6
85.0
135.5

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MgSO,  (total MgO equivalent 250.6 tons).  The approximate
inventory on December 27th, after 730 hours of operation,
was 73.9 tons of MgO and 329.6 tons of MgSO,  (total MgO
equivalent 196 tons).  The inventory difference of 54.6 tons
is attributed to process losses, approximately 150 Ib/hr.
This may be contrasted with 223.7 Ib/hr. loss sustained in
the final operational period of the New England S02 Control
Project.  As was the case in the oil-fired application, most
of these losses occurred from uncontrolled spills and bleed
streams at the regeneration plant; however, during this
period, November to January the regeneration plant only
operated a total of 226.3 hours accounting for the lower loss
rate during the PEPCO project.
     By the end of December the entire inventory had been
processed through an additional cycle.  Some limited runs
were conducted in January with 142 hours of two stage opera-
tion at Dickerson which initiated a new cycle of regeneration.
    At Rumford, 194 tons of MgSO, remaining from the New
England S02 Control Project had been in storage since July
1974.  The first rail car of this material (80 tons) was pro-
cessed with dryer product from Dickerson during January  1975
in a rate check of the calciner  feed capacity.(D
    An examination of the statistical summaries for the
Dickerson operations reveals a trend of a gradual increase in
unreacted MgO in the recycle liquor similar to that seen in
operations at Boston Edison's Mystic Station.
Period               MgO in Recycle (Avg.)     Standard Deviation
11/10-11/29                3.81%                   2.90
12/1-12/29                 3.95%                   3.10
1/11-1/27                  5.79%                   1.40
4.5 POST OPERATION FGD SYSTEM INSPECTION
    In January 1975, before the FGD system overhaul, the
   Due to lack of operations at PEPCO and eventual termina-
tion of the entire program the regenerated MgO never found use
at Dickerson Station.
                        - 69 -

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major pieces  of equipment in the plant were inspected to
determine their condition.  The scrubber vessel was found
to be in good condition with only a few, small internal
areas where its plastic lining had failed.  The fan was
found to be in excellent condition as was the secondary
mist eliminator vessel.  Most other equipment, vessels and
pumps in the system were in good to satisfactory condition.
Major failures and unsatisfactory conditions were noted for
the first and second stage recycle piping.  A report of
the inspection is given in Appendix 1.
    An operating history of the plant showing the number of
runs started and their duration is given in Table 15.
    Problems which had an adverse effect on operability of
the FGD system were divided into several catagories which
are described in the following sections.
4.5.1  1st Stage Piping
     Problems with some portion of the 1st stage piping sys-
tem were the most frequent cause of scrubber shutdowns and
accounted for about one-third of the total.  There are five
separate, but interrelated causes of failure that have been
recognized, as follows:  (a)  pulsation in the piping near
the inlet to the scrubber,  (b)  high liquid velocities at
some points in the system,  (c)  the presence of sharp ob-
jects in the system due to corrosion of stainless steel,
(d)  rubber lining thinner than specified, (e)  poor adhe-
sion of rubber lining to the steel pipe.
    (a)   Pulsation in the piping near the inlet to the
         scrubber caused several failures of the pinch
         valve liners.  The valves were finally replaced
         with rubber lined spool pieces.  The pulsation
         also contributed to the failure of the elbows
         just before the scrubber inlet in all three of
         the 6-inch lines to the center nozzle.  The cause
                     -  70  -

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                 TABLE 15
            OPERATING HISTORY

               FGD SYSTEM
Date
1973:
Sept.
Oct.
Nov.
Dec.
1974:
Jan.
Feb.
Mar.
Apr.
May
June
July
Aug.
Sept.
Oct.
Nov.
Dec .
Number Of
Runs Started

2
2
4
3

1
0
0
5
1
0
0
6
6
4
5
6
1975:
      Jan.
          TOTALS
3_

48
                                           Duration Of Runs,
                                                  Hours
  46

  90

 142

 249




 192

   0

   0

 174

 100

   0

   0

 248

 326

 344

 318

 420



 131

2,780
                    - 71 -

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      of the pulsation was eventually traced to the
     hydraulic design of the piping system.   The
     pressure drop between the high point in the sys-
     tem and the scrubber inlet was less  than the
     vertical distance/ resulting in an alternate fill-
     ing and emptying of the line.   Corrective action
     has been taken by the installation of restrictive
     orifices in each of the inlet pipes, immediately
     before entrance to the scrubber.  Also, new tan-
     gential nozzles have been designed for a higher
     pressure drop—sufficient to compensate for the
     head between the restrictive orifice plate and
     the nozzle outlet.
(b)   Excessive liquid velocities caused failures in the
     1st stage bleed control valve and in a 316 stain-
     less steel pipe section immediately  after the con-
     trol valve.  The corrective action taken (some-
     time prior to August 1974)  was the installation of
     three eccentric orifice plates in horizontal piping
     runs in order to increase the pressure at the down-
     stream side of the control valve, thus permitting
     the valve to operate in a more nearly open position
     with reduced velocities through (and immediately
     after)  the valve.  The eccentric orifice plates were
     designed for velocities that would be adequately
     low for normal conditions.   However, with the actual
     conditions, as will be discussed in  (c), (d) and
     (e), failures of the rubber lining occurred adjacent
     to and downstream from the eccentric orifice plates.
     The plates were removed, leading to  a recurrence of
     failures in and after the control valve.  Correc-
     tive action has now been taken by the installation
     of a concentric orifice flange at the short, vertical,
     discharge end of the line.

                - 72 -

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(c)   Sharp pieces of metal  were present in the liquid
     cycle on numerous  occasions as a result of cor-
     rosion failures of stainless steel as will be
     described in a subsequent part of this section.
     The adverse effects were aggravated by conditions
     to be discussed  in (d)  and (e).
(d)   The rubber lining  as supplied  was thinner than
     the 1/4" specified.   This was substantiated in
     December 1974 by micrometer measurements of rub-
     ber samples from five  locations, selected at ran-
     dom from pipe sections that failed.
     Readings, in inches, were as follows:
                              0.160
                              0.154
                              0.150
                              0.133
                             Average
     In every instance the original "waffle"  pattern
     was still on the rubber and there was no evidence
     of any erosion.   Replacement pipe linings have
     been a full  1/4-inch thickness and there have been
     no failures  of  any of the replacement linings.
(e)   Adhesion of  rubber lining to the steel has been
     poor.   This  has not been measured quantitatively
     but has been judged qualitatively by pulling por-
     tions of the lining from pieces that have failed and
     also by inserting a knife or fingernail  between steel
     and rubber flanges.  The significance of poor adhe-
     sion is that it allows a small failure to grow rapidly
     into a large one that cannot be controlled with ex-
     ternal patches.

                 - 73  -

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4.5.2  2nd Stage Piping
     Failures of second stage piping became quite extensive
in October 1974, and several replacements had to be made.
Portions of the 16-inch and 20-inch piping that wore were
repaired by applying a polyester or epoxy coating, rein-
forced with glass fabric to the thin area.
     Failures are ascribed to a combination of erosion and
corrosion.  For long-term commercial use it is planned that
rubber-lined piping will be specified.
     An extensive series of piping thickness measurements
were made in late December 1974, using an ultrasonic gauge,
with the primary objective of establishing which portions of
the piping system needed to be replaced (or covered) in
order to provide for three months of additional operation.
4.5.3  Corrosion of Stainless Steel
     During early operation of the scrubber there were a
number of failures of stainless steel elements fabricated of
type 304 or other types that are less corrosion resistant
than type 316.  Type 316 has performed with mixed results,
depending on the specific environment encountered.
     The first stage tangential inlet nozzles corroded and
failed.  It was concluded that the cause of failure in this
case was the condensation of strong sulfuric acid from the
flue gas onto the outer surface of the pipes—a mechanism
similar to that which has been encountered in air heaters
when flue gas is cooled to too low a temperature.  Replace-
ment nozzles were fabricated in both glass reinforced poly-
ester plastic and stainless steel coated with glass re-
inforced polyester.  Stress has been another cause of failure
of type 316 stainless steel exposed to first stage liquid
as evidenced by extensive attack where threads had been cut
or cold bends had been made.  This was particularly notice-
able in the case of bolts in the south thickener and hanger
rods supporting the first stage demister piping.
                      - 74 -

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     Replacements for the latter were heat treated after fab-
rication in order to prevent attack from this cause.
     In the absence of either undue stress or conditions that
permitted condensation of strong acid from flue gas, type
316 provided satisfactory performance.  Examples are the hold-
down straps for the mist eliminators, where there was general
light pitting but no measurable loss of thickness and short
sections of piping to the tangential nozzles, just before en-
trance to the scrubber, where thickness was very nearly equal
to specifications and there was no visual evidence of corro-
sion.
                      - 75 -

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     5.0  PERFORMANCE TEST RESULTS

     Performance tests of the particulate emissions and SO2
control system installed at Dickerson Station were conducted
by York Research Corporation.  The testing period extended
from August 26, 1974 through September 21, 1974 following a
preliminary period in September for equipment set-up,
familiarization, establishing gas velocity profiles and gas
flow measurement.
    The performance testing used methods detailed in the
Federal Register, Vol. 36, No. 247, 1974 for:
    a)   Gas Analyses by Method 3
    b)   Particle Sampling Outlet by Method 5
    c)   S02 Removal Efficiency by Method 6
    d)   SO, Determination by Method 8
    Particle sampling at the inlet was conducted in accordance
with ASME PT6-27 (modified).
    Sizing of the collected particle samples was done micro-
scopically.  This method is semi-quantitave as the actual de-
minsions measured are the diameter or length of the particle.
This gives a general indication of the particles size and a
mathematical approximation of its mass.
    The data have been abstracted from York Research Corpora-
tion 's Report Y-8513 dated January 31, 1975.
5.1 PARTICLE EMISSIONS
    Results of the particle emissions tests are summarized.
in Table ig.  Each result represents the average of four tests
per series.  Additional data are also provided on gas flow
and composition.
                     -  76  -

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                                 TABLE  16
                      PARTICLE  EMISSIONS TEST RESULTS
                                FGD  SYSTEM
Test(1> Boiler Load ESP(2) Xip(3) Flue Gas Flow
Series MW in H2O 103 ACFM
5A 183 Yes 10.2 299
i SB 96 Yes 11.1 161
-j
-j
6 185 Yes 10.6 153
7 183 No 10.7 282
8 176 No 10.0 127

Inlet
Outlet
Efficiency
Inlet
Outlet
Efficiency
Inlet
Outlet
Efficiency
Inlet
Outlet
Efficiency
Inlet
Outlet
Efficiency
Tgmp.
242
126
241
116
240
136
245
118
232
CO- 0- Gr/SCFD
% * 12% C02
12.2 6.5 0.190
0.002
99.0
11.9 6.7 0.101
0.005
95.0
12.3 6.4 0.120
0.007
94.2
11.9 6.5 3.654
0.014
99.6
11.6 7.1 3.276
0.017
99.5
Gr/ACF
0.131
0.002
98.5
0.070
0.004
94.3
0.085
0.007
91.8
2.474
0.011
99.6
2.212
0.014
99.4
Average of four  (4) tests per test series
Indicates whether  the flue gas treated by  the  scrubber  stage passed
through the electrostatic precipitator  (Yes) or not  (No).
First stage (scrubber) pressure drop.

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     As noted in Section 4.1 the conditions over which the
tests were conducted were varied to provide data on a range
of operational situations, taking gas either ahead of or
after the precipitator.
    These results show the low particle emissions attain-
able using the Chemico wet scrubber.  In the tests taken
after the precipitator outlet particle emissions were less
than O.Olgr/SCF for all cases despite the low inlet loading.
For the full boiler load, full gas flow case (5A) fly ash
emissions were less than 4 Ib./hr.  When the system was
tested without the precipitator scrubber particle removal
efficiencies of 99.5% plus were obtained.
    As the installation was designed to process only one-half
of the total gas flow from the boiler the results noted above
do not represent the actual stack emissions as this consists
of both the contribution from the scrubbed flue gas and the
particle load remaining in the unscrubbed portion.
    An estimate of precipitator efficiency can be obtained
from the test results by using the inlet loading to the test
series before and after the precipitator as a measure of the
inlet and outlet condition of the precipitator.  This esti-
mate is shown in Table 17.
     The improvement in the efficiency of precipitator
operations, as shown in Table 17, as the amount of gas flow
to it decreases was confirmed in a later series of tests
which showed an increase to 99% efficiency in the ESP when
the gas flow was divided equally between the scrubber and
the precipitator.
5.2 S0v EMISSIONS
      J^
    Results of the sulfur oxides emissions tests are sum-
marized in Table 18 and represent the average of four de-
                    -  78 -

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                    TABLE 17

                   ESTIMATE OF

      ELECTROSTATIC FBECIPITATOR EFFICIENCY
                                   Efficiency (Based)
  Boiler    Particle Load (Avg.)   On 3.6  GR/SCFD        Source
Avg. Load   Inlet        Outlet       Inlet load        (Test Series)
MW          Gr/SCFD      Gr/SCFD


183         3.654                                            7


183                      0.190         94.8%                 5-A


96                       0.101         97.2%                 5-B
                        -  79 -

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CO
o
                                     TABLE 18

                               SOX EMISSIONS TEST RESULTS

                                       FGD SYSTEM
Test
Series
5A
5B
6
7
8
pd)
in H2O
15.1
6.6
5.1
14.7
5,2
Inlet
779
1373
800
1418
1419
SO, (PPM)
Outlet
78
157
137
88
156
SO, Removal
^ %
90
88.7
82.9
93.9
89.0
SO,
Inlet
34.6

47.5
2.9
1.8
(PPM)
Outlet
3.56

3.31
0.64
0.41
              (1)
                 Second stage (absorber)  pressure drop.
              *Test results abstracted from York Research Corporation,

               Final Report, Y-8513, Jan. 31, 1975.

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terminations per series.  Except for tests series 5A
most results for SO, removal were reasonably close to the
average, in test series 5A removal efficiencies measured
in the individual tests ranged from 83.5% to 96.8%.
    In general, the trends noted by these results  (reduced
efficiency at lower pressure drop and lower inlet SO- con-
centration) are similar to those seen in the oil fired appli-
cation of this prototype FGD method.  The correlation de-
veloped from the New England S02 Control Project has been
used to analyze the data from this project.
    SO., inlet and outlet concentrations were also deter-
mined during the performance test series and show a signi-
ficant reduction across the two stage scrubber for both gas
taken before the electrostatic precipitator and the gas
taken after the electrostatic precipitator cases.
       Maryland State Department of Health and Mental
Hygiene 10.03.39 "Regulations Governing the Control of
Air Pollution in Area IV", maximum allowable emission
of particulate for all solid fuel burning installations
greater than 200 million BTU/hr. furnace are 0.03 GR/SCFD.
                    - 81 -

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                TABLE 19




REMOVAL EFFICIENCY FOR PARTICLE SIZE RANGES
Test
Series
5-1
5-2
5-3
5-4
Average
Removal Efficiency
Above 5^M
99.0
99.8
99.0
98.8
99.2
1 to
97
99
99
97
98
5 /KM
.5
.2
.9
.5
.4
Below l/t
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               TABLE 20
OQAL ANALYSES -  COMPOSITE TO BUNKER #3
DATE From
To
Total Moisture
Dry Volatile
Dry Ash
Dry S
Dry Btu
M&AF Btu
DATE From
TO
Total Moisture
Dry Volatile
Dry Ash
Dry S
Dry Btu
M&AF Btu
1974
11-1
11-5
6.03
22.58
21.85
2.36
11,684
14,951
12-18
12-24
12.40
22.99
17.53
2.42
12241
14843
11-6
11-12
5.93
22.31
20.43
2.36
11,826
14,862
12-25
12-31
7.90
24.66
15.51
2.41
12711
15044
11-13 11-21 11-27 12-1
11-19 11-26 11-30 12-10
8.67
21.58
19.11
2.15
12,096
14.954
1975
1-7
8.06
24.26
17.05
2.42
12467
15030
7.50
21.14
17.77
2.15
12,399
15,078
1-8
1-14
8.37
24.74
15.34
2.20
12809
15130
7.95
22.44
21.06
2.25
11,686
14,804
1-15
-121
3.18
22.21
13.09
2.26
13492
15524
9.66
23.36
19.23
2.13
11,934
14,775
1-22
1-31
8.19
25.12
17.80
2.06
12477
15142
12-11
12-17
10.69
25.18
19.50
2.17
11,911
14,796
2-1 2-5
2-4 2-11
8.70 9.78
23.67 24.62
16.68 16.09
2.28 1.88
12553 12514
15061 14914
           Randan Sample
Arsenic    13.6 ppm
Tellurium   1.4 ppn
Selenium    1.1 ppn
                   -  84 -

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         6.0  PROCESS CHEMISTRY

6.1 FIRST STAGE  (PARTICLE CONTROL) OPERATION
    While most attention was focused on the S02 removal
section of the system some work was done to determine the
composition of the various important streams in the first
stage liquor loop.  Tests were conducted during the perfor-
mance test work carred out in August and September 1974.
    These tests involved analysis for a number of chemical
species in the streams going to the first pond/ the first
stage bleed, thickener underflow and overflow, and the sump
pump discharge.  Components analyzed were calcium,
potassium, aluminum oxide, magnesium, chromium, cadmium,
titanium oxide, silica, sulfates, sulfites, and chlorine.
In addition, the pH and total dissolved solids were also
measured.
    In order to complete the data and provide some standard
of comparision a series of baseline analyses was done for
both the inlet and outlet of the pond system and the various
system water supplies during a period of limited activity of
the FGD system, prior to the inauguration of the performance
test work.
    The data for both the baseline period and the performance
test period have been abstracted for a number of streams and
arepresented in Table 21.   In these tests the baseline data
aregiven where available, while the compositions during the
testing period (samples were taken intermittently for the
period August 29 through September 21, 1974) are presented
as an average for all tests days for the first stage bleed,
the pond (Basin #1) inlet, and pond return  (Make Up Water to
Dilution Tank).
                    - 85 -

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                                            TABLE 21
                         Chemical Composition at Various Streams in the
                            First Stage - Fly Ash Removal System
Sampling
Point
First
Bleed
Inlet
Basin
Make
Water
Stage

to
#1
Up
to
Potassium
ppm
Avg. All Tests 24. 6

Baseline n.a.
Avg. All Tests 12. 9
Baseline 16.4
Avg. All Tests 10.9
Calcium
ppm
7.

11.
8.
10.
8.
8

4
8
1
8
Magnesium
ppm
562.

78.
755.
83.
123.
0

1
7
7
2
Iron
PPm
87.4

38.0
41.3
69.2
.4
Cadmium Copper Chromium
ppm ppm ppm
.94 1.2

.01 .23 0.6
.04 0.44
.01 2.42 0.64
.04 .08 .13
Mercury
ppb
12.7

2.0

2.0
4.7
Dilution Tank
Service
Water
Supply
Baseline
              n.a.
13.3
83.6
,07
.49
0.74
2.0
                                                - 86 -

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                  Table 21  (Cont'd)
Chemical Composition at Various Streams in the
   First Stage - Fly Ash Removal System
Sampling
Point
First Stage
Bleed
Inlet To
Basin #1
Make Up
Water To

Avg.
All Tests
Baseline
Avg. All Tests
Baseline
Avg. All Tests
Sodium
ppm
17.0

16.2

21.8
10.0
Flouride
ppm
1.4

1.0
1.5
1.0
1.9
SO.
ppm
4921.0

1.0
2024.4
408.1
597.8
Dilution Tank
Service
Water
Supply
Baseline


45.1


1.0


39.2


                                                     Phosphate
                                                        ppm
                                                        32.4
                                                         2.1
                                                        18.0

                                                        16.3
                                                         7.8
                                                         2.2
Cl
537.0
224.0
 64.2
                    - 87 -

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6.2 PROCESS CHEMISTRY
    In an aqueous  envirpnment the following series  of  reactions
can be envisioned  for S02 absorption by pulverized  solid
MgO:
     1.  Slaking of  MgO
nyu(s) + H2U(1)
Mr-r /OTM /rii-iln\ . .
S0_ Absorption
Of")
°°2 (g)
S02 (Soln) + H20 —

Formation of MgSO,
— ^MrrfnvH fQnlrO
+ 2 -
	 >Mn -4- 5OH
-*-gf^ f^r^l r\\
	 tail 4. IICO —
+ ^ -2
and Mg(HSO,),
\v-±)
(6-2)
(6-3)
I fi-4}
\\) 1 1
(6-5)
(6-6)
(6-7)
(6-8)
          Mg(OH)   (Soln)  + HS0  + (x-2)
                               x = 3 or 6
     Mg(OH)2 (Soln)  +  2H-
     MgSO, x H2O 	
     Mg(HS03)2 	
4.   Other reactions  (side):
-j — >Mg(HS03),+2

                                       +S0
                                           ,
           (  ^H20
           2HSO3-
co2 w ^ "2
-CO- (Soln; 	


                                 :O3 (Soln)
                                  + HC03-
                                  + C03-2
         2 MgS03 x  H20 + 0^—»2 MgS04 + x
         Mg (OH) 2 (Soln) +H2C03+3H2->'MgC02.5 H20
         Mg (OH) 2 (Soln)  + SO^-»-MgSO4 + HjO
(6-8)

(6-9)
(6-10)
(6-11)

(6-12)
(6-13)
(6-14)
(6-15)
(6-16)
(6-17)
                    -  88 -

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6.2.1  Absorber Reactions
     In the system the main reaction in the second or SO2
removal stage is the neutralization of H2SO3 by hydrated
MgO to form insoluble hydrated MgS03.  MgS03 crystallizes
out with either three or six molecules of water.  The
nature of the hydrate, i.e., hexa- or tri- is partially
dependent upon the temperature in the absorber.  (Hexa-
hydrate is stable at room temperature while the trihydrate
is stable above 108°F).  The transition temperature of the
two hydrates, according to the literature, is 42.5°C
(108.5°F).  During operations at PEPCO the temperature of
the recycle slurry averaged about 110°F.  Since this tem-
perature in the absorber is higher than the transition tem-
perature it was expected that the trihydrate of magnesium
sulfite would be the main product as was the case during
the work on the Boston Edison Project.  However, in actual
operation, at Dickerson Station the centrifuge cake
analysis showed almost 95%
                  - 89 -

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6.2.2  Formation of Oxysulfates
    At PEPCO feed MgO was digested in mother liquor that
has as its main consitutent magnesium sulfate in solution
(approximately 15% dissolved MgSO.).
    It is known that MgO may react with MgSO. solution to
form a jell like substance.  This jell consists mainly of
basic magnesium sulfate, represented as:  xMgS04 yMg(OH)2
zH-O.  The values of x, y, and z are dependent upon the
concentration of reactants and temperature.
    During early operations at PEPCO, when virgin MgO was
used in the unheated mixing tank considerable jell and lump
formations occurred.  X-ray and chemical analysis of these
products showed the presence of 3Mg(OH)2MgS0.8H20  (i.e.,
oxysulfate in varying amounts admixed with quantities of
unreacted Mg(OH)2•
    Laboratory studies, which were initiated to investigate
this problem concluded that:
    1)  The problem appeared to be confined to operation
        with virgin MgO particularly at high MgSO. con-
        centrations (15% MgSO, or more) in the centrate.
        The problem is further aggravated when the MgO-
        MgS04 mixture is allowed to stand for a time with
        insufficient agitation.
    2)  When calcined MgO  (regnerated) of bulk density
        above 20 Ib/ft  is used in the reaction no major
        problem was observed as long as proper agitation
        and temperature of digestion of virgin MgO were
        maintained.
    Because of lack of operating time the laboratory obser-
vations with regnerated MgO could not be completely confirmed
in the plant.
                   -  90 -

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6.3 MAGNESIUM SULFITE CHEMISTRY
    Fundamental questions in the Chemico Basic Magnesia
Slurry Process are the chemistry of the formation and de-
hydration of the hexa and tri-hydrate forms of magnesium
sulfite, and the mechanism of MgSO,-MgS04 thermal decom-
position in the presence of carbon and a reducing atmos-
phere.
    Understanding of the first would allow control of the
production of the hydrate type formed in the absorption
system thereby affecting economies in the separation and
drying of these materials.
    Knowledge of the second might lead to process improve-
ments for production of richer SO- off-gas, with more re-
active MgO, or direct conversion to elemental sulfur.
    Because of the complexity of these questions research
work in the three areas was divided between the Chemico
laboratory facilities at the Rumford, R.I., plant and the
New Jersey Institute of Technology,  (N.J.I.T.) Department
of Chemical Engineering and Chemistry.  Most of the instru-
ment studies, i.e., Mass Spectroscopy, I.R. Spectroscopy,
Differential Thermal Analysis, Thermogravimetric Analysis,
etc. were performed at N.J.I.T.  The results of these studies
are given in the Appendicies.
    The following section is a summary of the principal
findings resulting from the work.
6.3.1  Conditions Governing the Formation of Magnesium
       Sulfite Hydrates
    A literature survey showed the existence of only two
hydrates of magnesium sulfite:  MgS03.6H20 and NgSO^-
The hexahydrate is  more stable at ambient conditions.
The hydration energy of the two are as follows:
                    -  91  -

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     MgS03 +  6H20	->MgS03.6H20 -13.38 K Cal.
     MgS03 +  3H20  	>-MgS03.3H20 -11 k Cal.
    The N.J.I.T. study of the reaction of S02  (at 320°F)
with MgO slurry at  120°, 135°, 149° and 176°F showed that
at 120° and 135°F the major product was MgS03.6H20 while
the trihydrate, MgS03.3H20 was the  dominant product at
149° and 176°F.  Presence  of MgS04 in solution  (up to 18%)
and passage of excess air did not have any significant in-
fluence on the nature of the hydrate formed.
    At Rumford, the reactions of S02 (at 300°F) with MgO
(virgin and regenerated) were studied at 135°, 140-145°
and 150°F.  The pH was maintained at 6.8-7.20.  Samples
were collected periodically and the filtrates were returned
to the reactor.  The results of the study agreed with the
conclusions noted above.
    At 135 F the major product was the hexahydrate and tri-
hydrate was the predominant one at 150°F.  The study at
140-145 F was interesting—it showed the gradual change
from hexahydrate (original product) to trihydrate (final pro-
duct) .   The complete transormation of the hexahydrate to tri-
hydrate took place in 4-5 hours of run.  The study  (140-145°F)
also showed that the transition of hexahydrate to trihydrate
is accompanied by a reduction of crystal size  (from 200 to
50 micrometers).
    Analysis of centrifuge cakes from PEPCO and Boston sup-
port the validity of the contention that (a) the ratio of
the two hydrates at any temperature is controlled by the
equilibrium value at that temperature,  (b)  hexahydrate per-
sists even above the transition temperature and  (c)  the
rate of transition is slow (cf. Kovachev Ts. et al. f Khimiya
i Industriya.   Sofia 42 (5)  (1970) 209-211.   Transition
temperature of the hydrates, 40 C or 104 F).
                   -  92  -

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Centrifuge Cake From
Boston  (135°F)
2-20-74 to 2-21-74
                       Centrifuge Cake From
                       PEPCO (120°F)
                       12-10-73 to 2-15-73
Hours
Ratio of 3H20
         6H20
Hours
Ratio of 3H20
         6H20
 0             0/100                 24             16/84
 4             12.5/87.5             48             9/91
12             30/70                 74             11/89
16             37/63                 97             18/82
20             49/51                130             7.5/92.5
24             55/45
28             58/42
32             70/30
     The variation in PEPCO samples was probably due to tem-
perature fluctuations in the system (the PEPCO system did not
stablize at the time.  However, analysis of centrifuge cakes
at later dates always showed a preponderance of hexahydrate
in PEPCO cakes).
6.3.2  Dehydration of Magnesium Sulfite Hydrates
     DTA, TGA and DSC studies with the two hydrates of mag-
nesium sulfite, MgSO~ 6H20 and MgS03 3H20 showed that the
path of dehydration and temperature of dehydration are depen-
dent on the manner of heating, i.e., whether dehydration took
place in an enclosed vessel or open or flow-through vessel.
(Appendix 2).
For example:
                           CONDITIONS
DTA Study
MgS0  6H
        CLOSED
        Two endotherms
           observed
        (at 107° and 205°C)
         OPEN
         One endotherm
             only
         (at 90°C)
                   - 93 -

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                           CONDITIONS
 DTA Study          CLOSED                OPEN
 MgS03 3H20         One endotherm only    One endotherm
                       (at 205°C)            (at 160°C)
 TGA study also showed similar behavior of  the two hydrates:
                          CONDITIONS OF STUDY
 TGA Study          CLOSED               OPEN
 MgSO, 6H-0         Two endotherms       One endotherm
                    (at 125° and 220°C)  only  (at 70°C)
 MgS02 ^H2°         One en(*otherm        One endotherm
                    (at 200°C)             (at 100°C)
      This study also showed that TGA  (enclosed environment)
 can be used to determine quantitatively the amounts of  the
 two hydrates in a mixture of the two.  Presence of inerts
 (any substance which does not change weight between 175°
 and 400°C) does not interfere with the determination.
 The only potential interferring element relevant to mag-
 nesia process is MgSO. 7H2O  (~7H2° at 200°c)•  Tne ^n~
 terference by MgSO, 7H~0 can be easily avoided by washing
 the sample with absolute ethyl alcohol  (only MgSO. &H20
 dissolves).  The amounts of the two hydrates, in a mixture,
 are calculated as follows:
          %MgSO. 6H90 = % wt. loss at  175°C x 2 x 100
                                   50.9
          %MgSO^ 3H,0 = 100 x (% wt. loss at 400°C - wt.  % loss atl75°C)
               J                        34.10
Additional dehydration studies were carried out in the
laboratory.
                    - 94 -

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     The two hydrates were heated in a vacuum oven (12
inches of mercury) at 80°C (176°F) , 120°C  (248°F) and
150°C  (302°F) for extended periods of time.  Samples were
withdrawn at intervals and chemically analyzed.
     At 176°F and 248°F little or no change was observed
with MgS03 3H20 even after 25 days.  At 176°F the hexa-
hydrate changed to trihydrate after 2 days  (confirmed by
chemical and x-ray analysis) .  At 248°F the hexahydrate de-
hydrated to yield a hydrate of apparent composition
MgS032H20 after 21 days.
     At 302°F the hexahydrate changes to trihydrate within
two hours.  Holding the compound at this temperature results
in a continuous, gradual loss of water.  After 200 hours at
302°F the starting hexahydrate had an apparent composition
of MgS03%H20.  When starting with the trihydrate it appears
to be stable up to 48 hours at the 302°F temperature.  Then
it looses water rapidly to give the apparent hydrate
     The rates of dehydration of the two hydrates at 330°F
are also different the hexahydrate loosing water more
rapidly than the trihydrate.  The rates of dehydration at
330°F were studies using Ohaus moisture balance.  To form
the anhydrous salt, MgSO.,, containing 10% moisture at 330 F
following retention periods were necessary:
for  MgSO,6H20      10 minutes
     MgSO,3H20      25 minutes
The dehydration study indicates that the water molecules are
more strongly bound in the trihydrate than in hexahydrate.
6.3.3  Mass Spectroscopy of the Two Hydrates of Magnesium
       Sulfite vs. Temperature
     The two hydrates were heated from 35° to 400°C in a
                   -  95  -

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Finnigan Quadrupole 1015 mass spectrometer.  No other
species except SO- and EJO were observed.  The plot of
log  (80) vs. temperature showed that the two hydrates
decomposed in a similar manner  (under vacuum conditions) .
 (Appendix 3) .
6.4  PULVERIZATION
     The SO- removal capability of MgO in the Chemico
magnesia system is dependent on both intensive and exten-
sive properties of the regenerated material.
     Of the extensive properties, the size range of the
MgO particles returned for slaking is very important.  Ex-
perimental data indicate that grinding the calcined magnesia
increases its reactivity.  However, there is a limit to which
that reactivity can be increased.
     Laboratory data now indicate that a size range of -100
to +200 mesh (between 75 and 150 micrometers) is satisfactory
for recycled, regenerated magnesia.  This is shown in the
attached graph (Figure 3) •  The greatest increase in MgO
activity occurs when +50 mesh size particles are reduced to
-50 to +100 mesh, additional improvement in SO, removal is
obtained when size is reduced to -100 to +200 mesh.  Reduc-
tion to finer size has only a slight affect on activity in-
crease.
     The properties of regenerated MgO (shown in Table 22)
are determined by both calcining conditions and contaminent
level.
                   - 96 -

-------
                                  FIGURE 8



                 EFFECT OF PULVERIZATION ON S02 EFFICIENCY
           60
           50
      o
      2
      O
      z
      w
      H
      o
      H
      fe
      fa
      W
      O
      co
40
30
20
           10
                                UPPER
                      X
                      50      100             200

                           SCREEN SIZE (TYLER MESH)
                                                  300  325
(1)
   Measure  of uptake of S02  by measured quantity of regenerated MgO by

   the method described in "The Magnesia Scrubbing Process as Applied

   to an  Oil  Fired Power Plant" EPA 600/2-75-057 pg.  253 ff.
                                  - 97 -

-------
                       TABLE  22

PROPERTIES OF DIFFERENT FRACTION REGENERATED MgO

                  (SAMPLE NO.  PR-289)
Analysis
+50 Mesh
Fraction
-50 to
+100 Mesh
Fraction
-100 to
+200 Mesh
Fraction
-200 to
-325 Mesh
Fraction
Ground +50*
Mesh Fraction
to (-100 to
+200}  Mesh
%MgO

%MgS04

%MgS03

S02 Eff.
89.96

 1.73

 0.50

   13
89.46

 2.43

 1.42

   37
90. :2

 2.60

 1.33

   47
91.73

 2.35

 0.98

   48
        48
                        - 98  -

-------
    7.0  CORRELATION OF PROCESS DATA

     With the initiation of the planned operations program
process data were collected and recorded regularly.  In order
to assimilate, store, analyze and deseminate this information
efficiently, a computerized  method of handling the data was
employed.  As a result, it was possible to effect a real-time
feedback to the process or correlated and trend results at the
time they are most useful, along with accumulating the infor-
mation in a permanent data bank available for analysis and
retrieval.  The statistical computer program package utilized,
permits the use of the same format data file as input to a
wide range of sub-programs, including regression calculations,
x-y plotting, file listings, trend plots, etc.  This flexibility
reduced the number of files that needed to be maintained, and
provided speed advantages.
     Figure 9 illustrates the flow of information between
scrubber and calciner operating systems and the computer data
bank.  Operating conditions and analyses are entered on punch
cards on a daily basis for primary storage and transferred to
computer disk files for futher processing.  At monthly inter-
vals the following statistics were generated for all variables:
average, maximum, minimum, standard deviation, and a percent
change relative to a base period.  The final stage in the data
flow was the integration of the operating log and analysis
files, plus the inclusion of appropriate time lags  for the
scrubber and regeneration facilities to form single disk files
suitable for input to correlation and plotter computer programs.
The process data bank becomes the source of retrieval of pro-
cess information for continued analysis and for comparison with
                     - 99  -

-------
o
o

                                       PATA
T
T
                                                                            RLE
                           Process  DATA  FLow PIA
-------
results from other installations.
     The process correlations developed in the previous "New
England SO, Control Project", EPA Ref. CPA 70-114, were de-
veloped primarily using the data bank as input to a stepwise
multiple linear regression program.  This approach minimizes
the number of computer runs required to determine equations
that are statistically significant, prior to their evaluation
for consistency with observed data.  F ratio tests are em-
ployed to establish significance levels for testing of equa-
tion variables, and coefficients are calculated by least
squares techniques.  With respect to the SO- removal efficiency
correlation, log transformations were required by the regres-
sion program.  Continued investigation of mass transfer co-
efficient in this program may lead to the use of non-linear
programs.
     Normal excursions in the process variables are sufficient
to satisfy the required scope of the test program variation
in levels of operating data to fulfill the requirements of
this method of operations data analysis.
7.1  S02 REMOVAL
     A correlation relating S02 removal efficiency, pressure
drop and S02 inlet concentration had been developed during the
previous operation of the MgO system prototype on the oil fired
boiler.  Included in the formulation of the correlation were
data points from the performance testing of Dickerson.  The
data accumulated during the additional operation of this pro-
ject was used to improve the correlation based on the varia-
tions of S02 removal efficiency and other operating factors
which were observed.
7.1.1  First Stage S02 Absorption
     A series of tests were performed with the scrubber to
assess the SO- removal capability of the first (particle re-
moval) stage of the system.  Results of these tests are given
                     -  101  -

-------
in Table  23.  These  tests  showed  an  average  removal  efficiency
for the first stage  of  6.7%.
7.1.2  Effect of Pulverization of Regenerated MgO
     During the period  of  scrubber operation at  PEPCO  from
November  1974 to January   1975,  the observed S02  removal
efficiency varied more  than could be expected from normal
changes in operating conditions,  i.e., pressure  drop,  S0_  in-
let concentration, etc.  Efficiency  decreased approximately
10% in November before  recovering in December and  January.
The efficiencies were adjusted to constant operating condi-
tions and plotted to show that a significant variation in SO^ removal
remained  after adjustment  of pH and  pressure drop  which  was
assumed to be related to other process variables.  Figure  10
is plot of removal efficiency vs.  time illustrating  this
phenomenon.  The scale  of  the plot is expanded to  show the
effect more clearly.
     Laboratory studies indicated that a critical  particle
size range was required to maintain  activity of  the  regenerated
magnesia.  In order  to  determine  whether any relationship
existed between MgO  particle size distribution and S02 removal
activity  in the FGD  system, a series of MgO  samples  were taken
from the weigh feeder at Dickerson for screen sizing and
activity measurements.  Results of this analysis are shown in
Table 24 along with  corresponding scrubber operating condi-
tions for the time frame over which  the samples  were taken.
     This information was  analyzed by linear regression  tech-
niques and showed a  significant particle size correlation  with
SOj removal efficiency  in  the -50 to +100 mesh range.  The
correlation is given in equation  7-1.
             R =-7.68  - 0.0338 (P1QO)2            (7-1)
                R = % reduction in S02 removal efficiency
                                               material
                                               MgO Feed
Where PIOQ = %  (-50 to +100 mesh) material in
                     - 102 -

-------
Date

1/8/74
1/9/74
                TABLE 23
         0 REMOVAL IN FIRST STAGE
Time
1700
1900
2100
2300
2100
0300
0500
0700
0900
1100
1300
1500

Inlet
ppm
1300
1300
1390
1430
1300
1390
1500
1300
1070
1080
980
900
so2(1>
Outlet
ppm
1220
1290
1200
1340
1300
1360
1380
1300
990
900
900
800
                                               Efficiency
                                                    %
                                                  6.2%
                                                  0.8
                                                 13.7
                                                  6.3
                                                  0.0
                                                  2.2
                                                  8.0
                                                  0.0
                                                  7.5
                                                 16.7
                                                  8.2
                                                 11.1
(1)
                       Average Removal Efficiency 6.7%

Abstracted from the continuous emissions monitoring
data obtained using a Flourescent SO- analyzer.
                    - 103 -

-------
                                           FIGURE 10
o
*>.
A1*
D
J.

R
E.
M.

E
F
F.
19
10/.
4<
100 •
94 .
88 •
82 •
76 •
74
23 11/10 11/15 11/20 11/25 ll/
D 66 92 118 144 17
•
•
•
•
•

1

•
•»»••-••»
•*
•
• ••
•
• •
•
•
•


• •
• •• •
••
• •
•


•
•
•
••
• •••
•
•
•
•
•


•
•••
»••••••»
• •
• •
•
••
28 ll/
CLJLaS
• •
•
• ••
•
•
• •
•
•
• •
• •
•
'30



•
••
• ••
*•••
•
r '••
% SO0 REMOVAL EETICIEHCY VS. TIME 1975

12/7 12/9 12/14 12/17 12/20 12/22 12/29 1/13 1/25
2?0 26Q 29Q 320 350 380- 410 440 470 500 HRS./2


•
•
•
•
•
•
•
• •
•


•
• ••
• • •
•
•
••
•
•
•
•

•
•
• •
• ••
••
••
••
•
•*
••«»•••••
••
•
•

•
•
•••
• ••••
• •••• •
•• •
•
•
•


•
•
••
•• • •
•••• •
•
*
»••••••••


•
••
• •
• • ••
••

•
•
• •
••
•*
• *
• • •
•
•
•••

•
•
•
• •
• ••
•
•

•
• ••
•• •
•
•
•
•



•••••••••»

                  *Observed  SO2  ren.  eff.  ad-justed to conmon  basis of 9"^> P, 7 pH
                   1900 PPM  Inlet SO,.

-------
                                                       TABLE 24
                                              WET SCREEN ANALYSIS OF MqO BELT SAMPLES
Date (1974)
•Time
Tyler Screen
Mesh Size - %
+50
-50,+100
-100, +200
-200, +325
-325
£ Operating
w Conditions
1 P, In. H2O
SO2 Removal
Eff.,%
SO, Inlet
Cone. , PPM
Predicted (2)
SOj Removal
Efr. - %
(Actual-Predicted)
Efficiency/ %
11/20

1.0
0.8
2.6
4.1
91.5
(1)
9.5
85.1
1210.

85.0
0.1
11/21

0.8
0.5
1.5
2.2
95.0
(1)
9.3
86.2
1240.

85.0
1.2
11/24

0.5
0.6
1.3
2.7
94.9
(1)
8.9
83.8
910.

84.9
-1.1
11/25

0.3
0.8
1.7
3.3
93.9
(1)
8.2
84.1
920.

84.6
-0.5
12/1

4.6
14.5
8.2
6.9
65.8
(1)
6.4
76.0
1080.

76.4
-0.4
12/9
0800

5.2
5.4
12.2
11.8
65.4
4.2
79.0
1170.

79.5
-0.5
12/18
2000

3.6
5.7
10.3
13.8
66.6
8.4
82.0
1200.

83.5
-1.5
12/20
1200

6.6
6.8
13.3
10.1
63.2
3.6
80.6
960.

77.0
3.6
12/23
0400

0.7
1.9
7.7
13.6
76.1
8.5
83.6
840.

84.6
-1.0
12/27
1200

1.
2.
3.
2.
89.
5.
83.
900.

82.
0.

8
5
6
5
6
9
0


9
1
(1)
   Average Conditions For Day
(2)
  Fr°m Equation 7-1

-------
     After determining the pulverized MgO particle size the
resultant correction can be subtracted from the efficiency
obtained from the correlation developed from the previous
operations.  This basic correlation is given in equation 7-2.
     S02 Removal = 1-Exp ((2.666 (AP)A (S02I)B(10)C -3)) 7-2
     Efficiency  (Base)
        Where A = -1.014
              B = -3.75 + 0.271 In S02I
              C = 6 - 0.031 pH
          SO~T  - SO- inlet concentration (ppm)
            AP = pressure drop, inches H-O
     Figure 11 is a plot of the.predicted effect of the con-
centration of -50, +100 mesh size in the MgO on S02 removal
using equation 7-1 at constant process conditions.  Results
show that SO- removal decreases with increasing concentration
of this size range, which is consistent with laboratory obser-
vations.  Figure 12 is a plot of observed vs. predicted
efficiency during the subject time period.
7.1.3  Reduction in Activity of Magnesia
     Equation 7-1, showing particle size effect also predicts
a 7.68% offset from removal efficiency calculated from 7-2,
a correlation based on AP,  pH, and inlet S02 concentration.
     An analysis of inventory records during the period covered
by the testing program revealed that the magnesia feed consis-
ted of a mix of virgin and regenerated MgO.  The beginning in-
ventory on October 18th  at Dickerson was 46 tons of regenerated
MgO in the following week 140 tons of virgin MgO were added as
makeup to the silo.  About 22 tons of regenerated MgO were re-
turned to Dickerson in the period from October 18th through
November 29th while about 120 tons of MgO were consumed in the
operations there.  Thus during the period of reduced efficiency
virgin material was the principal feed to the system.  A
comparison of the manufacturer's analysis, Table  25,
                     -  106  -

-------
                             FIGURE 11
w
H
o
H
w

1
a-
O
CO
    86
    84
       EFFECT OF MgO PARTICLE SIZE ON SO., REMOVAL EFFICIENCY



              BASIS;  PEPCO Operation Nov.-Dec. 1974

           Adjusted to 7"   A P,  7 pH, 1000 PPM S02 Inlet
    82
    80
    78
    76
    74
                                6
                                                10
12
14
                      % (-50,  +100)  MESH MgO
                             -  107  -

-------
                              FIGURE 12
   88
   86
U

§  84
M
U
W
f^4



g
o
W

Q
W
EH
U
   82
   80
   78
   76
   74
           OBSERVED  VS.  PREDICTED S00 REMOVAL EFFICIENCY
           ^	£
       74
76
78
80
82
                                                 84
                                          86
                                          88
               OBSERVED SO2 REMOVAL EFFICIENCY -  %
                              - 108 -

-------
             TABLE  25
MANUFACTURERS ANALYSIS OF MAGNESIA
   SHIPPED TO DICKERSON STATION

CaO
SiO2
R2°3
Cl
so3
-325 M
LOI
S.A.
7/12/74
L&N200196
1.62
0.7
0.51
0.18
0.69
99.75
6.22
66.7
8/20/74
L&N200487
1.78
0.60
0.54
0.26
0.78
99.09
5.46
52.4
10/7/74
L&N200257
1.94
0.61
0.43
0.12
0.67
98.71
4.33
79.3
10/25/74
L&N200304
1.96
0.62
0.70
0.19
0.64
99.61
4.57
94.7
        Where R2^3 = Iron an(* aluminum oxides
            -325 M =  Percent less than 325 mesh
              LOI  = Loss on ignition
              S.A. = Surface area
                 - 109 -

-------
 for the virgin MgO supplied during the period of the
 program showed little deviation from that supplied at the
 beginning of the Development Program.
     It has been noted  (Sec. 6.3.4) that analysis of
materials from the MgO slurrying system in the earliest phase
of the project showed that the highly reactive virgin MgO
exhibited a stronger tendency to form magnesium oxysulfates,
which would hinder the S02 absorption efficiency of the
magnesia slurry.  It is thought that the deviation noted
here is a measure of the additional reduction in efficiency
resulting from the formation of the complex when a feed of
virgin MgO is admixed with centrate.
7.2  CENTRIFUGE OPERATION
     Centrifuge operations at both PEPCO and Boston Edison
were compared and analyzed with regard to process optimiza-
tion.  The effect of centrifuge feed rate on efficiency and
solids removal rate was determined by regression analysis of
the operating data.  Since the two centrifuges are mechanically
identical, it would be expected that similar operating charac-
teristics would be observed, and this was confirmed by analy-
sis.  The following results were obtained:
     1.  Centrifuge efficiency, i.e., pounds solids re-
         moved in centrifuge cake per pound solids in
         centrifuge feed, was shown to be a function of
         centrifuge feed rate with efficiency declining
         with increasing throughput.
     2.  Solids removed from the system was shown to pass
         through a maximum value as total feed rate to the
         centrifuge is increased.
Figures 13 and 14 show these results for centrifuge operation
with average recycle compositions, normal rotational speed
and standard weir height.
                    -  110 -

-------
                                          FIGURE  13


                 EFFECT OF CENTRIFUGE FEED RATE ON SEPARATIONAL EFFICIENCY
    80 --
dP
B
B
W
H
u
H
h
Cn
W
§
H
EH
H
(0
    70 - -
                                               BOSTON
                                PEPCO
60
     50
     40 --
     30
                  40
                         60          80       100

                              CENTRIFUGE FEED RATE GPM
120
180
160

-------
 m
O
03

s
Q

>H

as
     80
     70
g   60

S
    50
W   40..
    30
    20
     10
                               FIGURE 14




                         CENTRIFUGE OPERATION



                LB./MIN. SOLIDS SEPARATED VS.  FEED RATE
BOSTON EDISON
                    50
                              100                  150




                      CENTRIFUGE FEED  RATE (GPM)
200

-------
7.3  DRYER OPERATION
     Data from the operations at PEPCO were analyzed to
determine the influence of dryer operation conditions on
dryer efficiency.  A scatter plot of dryer solids vs. pro-
duct temperature is shown in Fig.15.  In addition, the data
collected during the Boston Edison operation were analyzed
and compared.  The results of preliminary review of the
effect of dryer product and dryer outlet gas temperature
on product moisture content is shown in Fig. 16 .   Variations
in the performance of the dryers is attributed to the use
of a counter-current unit at Boston and a co-current unit
at PEPCO.  A statistical analysis of this data shows a
minor interaction between dryer product and dryer outlet
gas temperature.
     An analysis of the change in the ratio of MgSO. to
MgS03 in the dryer feed and product streams, an indication
of oxidation accurring in the dryer, showed a slight decrease
in the MgSO^ concentration for PEPCO operations as compared
to the oil fired boiler application for the average range of
system operations.  This is  shown in Figure 17 .
7.4  CALCINER FEED RATE
     A limitation on reliable operation of the integrated
plants was reduced calciner feed rate.  A low (40 Ib/min.)
feed rate was necessary to control slides and unprocessed
MgS03 in the calcined product, Fig.18.  Initial investigations
during the work at Mystic Station indicated a relation be-
tween particle size of the dryer product and frequency of
slides.  Further investigation showed that variation in size
distribution of the dryer product was associated with varia-
tion in moisture content of the product.  During the final
phases of the program at Boston the dryer was operated to
produce a product with a moisture content of approximately
                    - 113 -

-------
                                          FIGURE 15
       100
in
Q
M
ij
O
en
Q

<#>
        90
        80
        70
          100
                      COMPARISON OF PEPCO AND  BOSTON EDISON DRYER OPERATION

                          (FOR RANGES  OF DRYER GAS OUTLET TEMPERATURE)
                         PEPCO DRYER
                                                           BOSTON EDISON DRYER
150
200          250          300



    DRYER PRODUCT TEMPERATURE,°F
                                                                            350
400

-------
  1014.33 —
   97.06
   89.80 _
   82.53 —
I
<*>
                                        DRYER OPERATION




                                         PEPCO DATA


                                           3/31/75
   75-27
    68.66.
         210.00
2U2.66
28l«. 96
I
326.00
368.00
U16.66
                            OUTLET GAS TEMPERATURE  °F
                                        - 115 -

-------
                          FIGURE  17
           COMPARISON OF MqS03  OXIDATION IN DRYER
 EH
 U
 D
 Q

 §
 On

 OH
 U
 S3
 H
  16




  14



  12




  10




   8
 n
O
en
O
I6
     BOSTON  EDISON DATA
PEPCO DATA
                                            t	l_
              2    4    6     8    10   12    14   16
                   MqSO.
                   MgSOj
                           IN DRYER FEED
                          - 116 -

-------
                            FIGURE 18
               CALCINER OPERATIONS ON PEPCO MgS03


             EFFECT OF FEED RATE ON MqS03 IN PRODUCT
      40
U



I
O
CO

3

OP
      30
      20
10
        45
            50
55
60
65
                   CALCINER FEED RATE LB/MIN.
                             - 117 -

-------
16% which eliminated the slides in the calcination step.
The investigations at Dickerson showed there was a signi-
ficant difference in the size distribution of the product
produced from its dryer compared to material produced at
Boston as shown in Tables 26 and 27.
     Table 26 shows the average values and standard devia-
tions for 25 Boston dryer samples and 22 PEPCO dryer sam-
ples covering the following mesh size ranges:  +25, -25,
to +50 -50 to +100 and -100 to +200.  Table 25 presents
a statistical analysis of these results.
                    -  118 -

-------
             TABLE 26
SIZE DISTRIBUTION OF DRYER PRODUCTS

Mesh Size
Range
+25
-25, +50
-50, +100
-100, +200


BOSTON AND
Mesh Size
Range
+25
-25, +50
-50, +100
-100, +200
BOSTON
25 Samples
Average Std .
58.1
14.9
9.4
4.7
TABLE 27
COMPARISON OF
PEPCO SIZE RANGE
Significance
Level
99% +
99% +
99% +
99% +
PEPCO

Deviation Average
10.2 22.3
4.5 29.5
4.4 23.5
2.0 11.1


AVERAGES
Difference
(Boston-PEPCO)
35.8
14.6
14.1
6.4
22 Samples
Std. Deviation
11.4
8.5
8.4
4.0


99% Confidence
Limits
27.2-44.5
9.2-19.9
8.8-19.4
3.9-8.9
                  -  119  -

-------
               8.0  DATA

8.1   MONTHLY AVERAGE OPERATING CONDITIONS
      Operating data are summarized as montly averages for
the planned operational testing period.  Included in this
information are:
      Table 28  Operating Conditions for the FGD System
      Table 29  Stream Compositions for the FGD System
      Table 30  Operating Conditions for the Regeneration
                Unit
      Table 31  Stream Composition for the Regeneration
                Unit
8.2   DATA LISTING
      Data recorded from the PEPCO operations for the
period October 15, 1974 through the end of the program in
January 1975 are given in Table 32 .   Data were  recorded  at
two hour intervals, which is the interval between successive
listing in the table for extended runs.
                  - 120 -

-------
                TABLE 28

 OPERATING CONDITIONS FOR THE FGD SYSTEM
MONTHLY
VARIABLE
S02 (PPM)
IN
OUT
% REMOV
PH
POWER PLANT
RATE (MW)
DIFF. PRESSURES
(IN. H20)
TOTAL
MIST
DRYER
TEMPERATURES (F)
-ABSORBER
INLET
MAGNESIA SLURRY
-DRYER
GASOUT
PROD.
FLOWS (GPM)
CIRC.
CENTFD
DATA AVERAGES
11/74
1057.86
193.46
81.54
7.04
174.03

7.49
0.23
0.76

109.26
157.02
274.65
179.36

10152.78
72.74

12/74
1061.95
207.90
80.57
7.06
153.98

6.77
0.19
0.69

110.88
139.20
311.03
200.62

10823.13
83.09

1/75
1272.22
214.89
81.95
7.11
142.82

6.49
0.21
0.80

108.54
130.33
254.11
165.30

11546.30
154.61
CENTRIFUGE
TORQ.
34.75
40.38
43.94
                     - 121 -

-------
               TABLE 29
STREAM COMPOSITIONS FOR THE FGD SYSTEMS
MONTHLY
VARIABLE
DRYER
% SOL.
% MgSO3
% MgS04
% MgO
CENTRIFUGE
% SOL.
% MgS03
% MgS04
% MgO
RECYCLE
% SOL.
PH
-FILTRATE
% MgS04
-CAKE
% MgO
MOTHER LIQUOR
% SOL.
-CAKE
% MgO
DATA AVERAGES
11/74

93.63
68.06
8.28
4.78

88.86
41.78
4.44
3.06

6.98
7.17

17.05

3.81

2.46

6.14

12/74

96.94
68.12
9.08
6.82

88.33
42.81
4.86
3.03

10.90
7.30

18.95

3.95

4.80

5.68
                                                    1/75

                                                    91.30
                                                    66.45
                                                     7.70
                                                     7.78

                                                    88.45
                                                    42.19
                                                     4.02
                                                     5.25

                                                     8.72
                                                     7.22

                                                    13.13

                                                     5.79

                                                     2.20

                                                     9.73
                    -  122  -

-------
                  TABLE  30
OPERATING CONDITIONS FOR THE REGENERATION  UNIT
            MONTHLY DATA AVERAGES

  VARIABLE            10/74      11/74      12/74      1/75
  CALCINER
     -TEMPERATURES (F)
      MDKILN           1260.59    1361.25    1451.97    1494.86
      GASOUT           571.75      534.04     544.39     582.89
      PRODEX           224.72      160.00     155.22     169.74
  -SOLID FLOWS (PPM)
     MgS03              50.20       51.62      56.61      55.40
     COKE                0.43        0.32       0.30       0.31
  NEUT. pH LIQ.          5.25        5.83       6.01       6.40
  ACID PLANT
  FEED GAS (%)
    02                   5.76        7.34       7.57       7.40
                       - 123 -

-------
                  TABLE 31
STREAM COMPOSITIONS FOR THE REGENERATION UNIT
         MONTHLY DATA AVERAGES

  VARIABLE            10/74      11/74     12/74     1/75
  CALCINER FEED
% H20
% MgS03
% MgS04
% MgO
% CARBON
11.20
64.08
7.89
5.80
2.66
11.38
67.47
7.25
4.94
1.35
6.00
63.78
9.25
7.69
1.76
6.45
68.42
8.63
6.28
1.32
  CALCINER PRODUCT
     % MgS03           0.45       0.15      0.92      0.46
     % MgS04           0.90       1.29      1.08      3.74
     % MgO            89.78      94.62     93.57     93.41
  BULK DENSTIY        27.61      22.73     22.41     21.31
                       -  124  -

-------
                   TABLE 32

          RUN DATES AND DATA LISTINGS



         RUN DATES
STARTING
10/15/74
11/24/74
12/6/74
12/14/74
12/27/74
1/12/75
ENDING
10/18/74
12/1/74
12/10/74
12/23/74
12/29/74
1/14/75
CASE NO.'S
1-31
128-214
218-277
279-384
386-415
421-451
The following identifies the abbreviated words on
Pages 126 - 133:
S02 IN PPM

% S02 REM

D GAS T

D PROD T

CIRC GPM

FAN AMPS
Parts Per Million Of SO- Into Scrubber

Percent S02 Removed In Scrubber

Dry Gas Temperature

Dry Product Temperature

Recycle GPM

Current required To Drive Fan
                    - 125 -

-------
       CASE NO.  i S02INPPM  2 isoz REM  3 PH
4 DELTA P   50 OAS T   60 PROD T  7 CIRC 0PM  8 FAN AHPS
N>
at
1
2
3
4
5
6
7
8
9
10-
1L
12
13
14
15
16
17
18
19
20
21
23
24
25
26
27
28
29
30
31
32
33
34
35
36
37
38
39
40
41
42
«3
44
45
46
4T
48
49
50
51
52
53
54
55
56
57
MISSING
MISSING
MISSING
MISSING
MISSING
MISSING
MISSING
MISSING
MISSING
MISSING-
MISSING
MISSING
MISSING
MISSING
MISSING
MISSING--
MISSING
MISSING
MISSING
MISSING
MISSING
U ¥ CC T Mf
HISSING
MISSING
MISSING
MISSING
MISSING
MISSING
MISSING
MISSING
MISSING
MISSING
**ISS[NG
MISSING
MISSING
MISSING
"ISSING
MISSING
"ISSING
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MISSING
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11 10.0000
1760.0000
1?60.0COO
1360.0010
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[?60.0000
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1360. 3000
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MISSING
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- MISS-ING- —
MISSING
MISSING
MISSING
MISSING
MISSING
tl T C C T U^
MISSING
MISSING
MISSING
MISSING
MISSING
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MISSING
MISSING
MISSING
MISSING
MISSING
BUSSING
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94.5900
9'. 8 100
93.9100
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7.3000
7.2000
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6.9000
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6.9000
6.9000
T 1 A A A
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7.1000
6.9000
7.0000
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7.1000
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6.8000
6.7000
6.9000
6.7000
6.9000
6.8000-
7.1000
7.1000
7.0000
6.3000
6.3000
6.9000
6.9000
6.7000
6.9000
6.9000
6.9000
7.0000 -
6.8000
6.9000
7.3000
7.3000
7.3000
7.4000
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MISSING
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6.6000
7.1000
6.9000
6.9000
6.7000
6.8000
6.3000
4.0000
9.0000
8.6000
9.0000
6.0000
5.6000
5.5000
5.0000
5.5000
5.5000 	
5.5000
5.5000
5.5000
5.5000
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5.5000
6.0000
5.2000
5.5000
5.5000
ff C A A A
-- - 5.5000
5.5000
4.0000
5.5000-
3.5000
'4.0000
4.5000 	
3.5000
3.5000
3.3000
7.0000
4.0000
9.0000
8.0000
8.6000
8.6000
8.6000
8.6000
8.6000 --
7.0000
7.0000
7.0000
8.5000
10.5000
13.4000
13.2000
MISSING
MISSING
2.5000
1.4000
1.5000
3.0000
3.0000
4.8000
2.0000
6.5000
MISSING
MISSING
MISSING
MISSING
240.0000
300.0000
380.0000
330.0000
280.0000
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150.0000
145.0000
160.0000
160.0000
170.0000
10000.0000-
9800.0000
10000.0000
9800.0000
9800.0000
10000.0000
10000.0000
10000.0000
10000.0000
-270-.0000 — -'175vOOOO — JOOOOvOOOO 	
240.0000
240.0000
255.0000
220.0000
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-32Or«000-
275.0000
280*0000
280.0000-
280.0000
360.0000
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220.0000
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225.0000
225.0000
-225.0000-
235.0000
235.0000
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210.0000-
220.0000
250.0000
240.0000
235.0000
235.0000
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210.0000
210.0000
210.0000
225.0000
225.0000
210.0000
260.0000
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265.0000
220.0000
270.0000
300.0000
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2T5.0000
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175.0000
165.0000
- 165.0000
160.0000
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1 O^ Aft Art
1*93* Uv VU
180.0000
180.0000
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170.0000
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	 165-.0000
185.0000
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-165-.0000
160.0000
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165.0000
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155.0000
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- 155.0000
165.0000
170.0000
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160.0000
160.0000
160.0000
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168.0000
177.00CO
180.0000
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165.0000
170.0000
185.0000
185.0000
190.0000
175.0000
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10050.0000
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9900.0000
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9800.0000
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12400.0000
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230.0000
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200.0000
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180.0000
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210.0000
180.0000
225.0000 	
225.0000
220.0000
220.0000
220.0000
220.0000
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220.0000
220.0000
220.0000
220.0000
240.0000
280.0000
280.0000
150.0000
150.0000
160.0000
150.0000
150.0000
165.0000
175.0000
190.0000
150.0000
220.0000

-------
10
vj

NO.
53
59-
60
61
62
63
64
65
66
67
66
69
70
71
72
73
74
75
76
77
78
79
80
81
82
83-
84
85
86
87
88
89
90
91
92
93
94
95-
96
97
98
99
100
101
102
103
104
105
106
107
108
109
110
111
112
113
11*
115
116
117
118
'« Z
1 S02INPF-
MISSING
— MISSING- -
MISSING
MISSING
MISSING
MISSING
MISSING
11*0.0000
1200.0000
1?00.0000
870.0000
1080.0000
MISSING
MISSING--
MISSING
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900.0000-
900.0000
960.0000
960.0000 -
900.0000
960.0000
1020.0000
1020.0000
960.0000
960-.-0000- "
960.0000
960.0000
1140.0000
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1260.0000
900.0000-
960.0000
900.0000
940.0000
1080.0000
900.0000
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900.0000
900.0000
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1080.0000
1080.0000
1020.0000
960.0000
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780.0000
1560.0000
1380.0000
1380.0000
1180.0000
1320.0000
1140.0000
1140.0000
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1140.0000
1140.0000
1140.0000
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sso2 REM
• -
rflSSINF
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77.8900
79.0000
79.5000
75.8600
84.4400
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83.3300
82.0000
80.6300
77.5000
86.6700
83.1300
85.2900
84.1200
80.0000
64.3800
81.2500
81.2500
81 .0500
78.5000
80.0000
76.6700
79.3800
79.3300
80.1200
80.5600
84.0000
86.4300
86.6700
86.6700
86.1100
86.1100
86.1100
79.4100
79.3800
7^.0000
MISSING
85.3800
MISSING
86.9600
86.9600
8*. 9600
8*>.3600
84.7400
3&.210D
84.3500
S3. 3300
8*. 2100
84.2100
MISSING
8*.2100
                                                    3  PH
4
6.6COO
7.3000
7.3000
6.5000
6.8000
6.8COO
7.1COO
6.7000
6.8000
6.6000
8.0000
7.2000
6.7000
7.6009 	
7.6000
7.5000
7.0000
7.1000
6.9000
O.VOOO
7.0000
7.2000
7.3000- '
7.1000
7.3000
7.5000 	
7.5000
7.5000
7.1000
7.2000
7.0000
7.0000 -
7.0000
6.9000
7.1000
7.0000
7.2000
7.3000 	
7.2000
7.1000
6.8000
6.8000
7.1000
6.8000
6.8000
7.2000
7.3000
7.1000
6.8000
7.1000
7.1000
7.1000
7.2000
6.9000
7.1000
7.1000
7.1000
7.0000
7.0000
7.0000
7.?000
DELTA P '
5.5000
6.200D
6.2000
1.000
3.5000
3.5000
4.0000
2.5000
4.2000
5.0000
6.0000
6.0000
4.0000
3.0000-
3.0000
3.0000
6.5000
5.0000
'• D GAS T—
MISSING
-- MISSIMG
MISSING
260.0000
283.0500
282.0000
252.0000
3] O.OGOO
230.0000
265.0000
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265.0000
—260.0000 -
310.0000
310.0000
295.0000
290.0000
5.2000 300.0000
^ _ A4WIA ^t A AAA.A
3 1 ruuuO 	 270 vO OOw ~
7.0000 300.0000
7.0000
8.3000
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- STIOOOO-
8.0000
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5.8000
3.0000
3.0000
5.2000
5.2000
7.0000
7.0000
7.0000
9.4000
12.0000
13.0000
12.5000
11.5000
11.5000
9.5000
M.ISSIN6
5.0000
1.2000
7.0000
9.5000
7.0000
9.2000
9.2000
9.2000
10.000
10.000
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8.5000
10.000
10.000
10.000
10.000
10.000
270.0000
310.0000
285.0000
300.0000
-- 260.0000 -
260.0000
260.0000
340.0000
MISSING
315.0000
315.0000
290.0000
300.0000
310.0000
300.0000
280.0000
245.0000
225.0000
280.0000
270.0000
270.0000
250.0000
200.0000 •
240.0000
238.0000
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MISSING
250.0000
255.0000
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240.0000
250.0000
300.0000
200.0000
200.0000
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200.0000
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'.62.0000
162.0000
180.0000
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175.0000
165.0000
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7 CIPC GPM
12400.0000
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10000.0000
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12000.0000
11700.0000
12000.0000
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155.0000
155.0000
160.0000--
175.0000
9100.0000
9300.0000
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9400.0000
165.0000 9400.0000
	 17-3vOOOO 	 9400-.0000 —
170.0000 MISSING
170.0000
18C.OOOO
182.0000
185.0000
- 185.0000---
155.0000
135.0000
190.0000
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195.0000
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170.0000
175.0000
135.0000
190.0000
188.0000
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182.0000 	 MISSING-
186.0000
200.0000
190.0000
190.0000
190.0000
- 160.0009- •
150.0000
155.0000
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175.0000
175.0000
180.0000
140.0000
130.0000
130.0000
170.0000
195.9000
1=0.0000
190.0000
150.000C
150.0000
140.0000
MISSING
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8500.0000
8200.0000
8600.0000
8600.0000
8600.0000
8600.0000
9500.0000
11200.0000
11200.0000
11200.0000
10400.0000
10700.0000
11100.0000
11100.0000
11300.0000
8 FAN AMPS
200.0000
220.0000 —
200.0000
:fo.oeoo
190.0000
18C.CCOO
200.0000
175.0000
190.0000
190.0000
220.0000
220.0000
200,0000
- 170.0000 —
180.0000
210.0000
220.0000-
200.0000
210.0000
— 175-5-00OO —
220.0000
220.0000
240.0000—
230.0000
200.0000
--235>-0000 	
250.0000
230.0000
200.0000 -
170.0000
170.0000
200.0000—
200.0000
220.0000
220.0000
MISSING
250.0000
280.0000
300.0000
300.0000
280.0000
280.0000
260.0000
240.0000 • -
180.0000
160.0000
240.0000
260.0000
240.0000
260.0000
260.0000
260.0000
260.0000
260.0000
230.0000
230.0000
260.0000
2*0.0000
260.0000
260.0000
270.0000

-------
to
GO
NO.
119
120
121
122
123
124
125
126
127
128
129
130
131
132
133
134
135
136
137
H8-
139
140
141
142
143
144
145
146
147
149
1*9
150
151
152
153
154
155
156
157
158
159
160
161
162
163
164
1«>5
166
io7
158
169
170
171
172
173
i7»
1^5
176
177
173
179
1 S02IKPPM 2 SSO2 REM 3 PH 4
114Q.OOOO
1140.0000
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MISSING
900.0000
1?00.0000
1680.0000
1680.0000
960.0000
960.0000
900.0000
900.0000
900.0000
900.0000- -
MISSING
MISSING
900.0000
960.0000
960.0000
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900.0000
900.0000
900.0000
900.0000
960.0000
960.0000
900.0000
900.0000
900.0000
960.0000
960.0000
1020.0000
1020.0000
1020.0000
1020.0000
1020.0000
1020.0000
060.0000
1080.0000
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1020.0000
1020.0000
1080.0000
1140.0000
1140.0000
1140.0000
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79.4700
79.4700
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81.3300
92.0000
94.6400
94.6400
81.&800
81.8800
82.0000
85.3300
85.2200
84.4400
MISSING
MISSING
82.6700
82.5000
85.6300
84.0000
84.0000
84.6700
84.6700
84.0000
84.3800
84.3800
82.0000
82.0000
83.3300
83.1300
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82.3500
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82.9400
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80.6300
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81.1800
81.1800
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30.5600
80.5300
80.5300
79.4700
70.2400
73.3300
7°. 3300
30.0000
6'.9403
00 	 9300.0000 	
MISSING
MISSING
215.0000 -
203.0000
230.0000
— 228. -00 00 	
230.0000
220.0000
250.0000
265.0000
272.0000
240. -0000—
210.0000
220.0000
220.0000
220.0000
240.0000
230.0000 	
230.0000
230.0000
230.0000
230.0000
270.0000
290.000&
300.0000
280.0000
2*0.0000
220.0000
220.0000
230.0000
230.0000
225.0000
220.0000
220.0000
220.0000
225.0000
220.0000
220.0000
220.0000
220.0000
?25.0000
230.0000
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240.0000
240.0000
240.0000
310.00CO
155.0000
160.0000
155.0000
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172.0000
163.0000
172.0000
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173.0000
160.0000-
160.0000
158.0000
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159.0000
1-70.0000
170.0000
170.0000
170.0000
170.0000
180.0000
180.0000
180.0000
185.0000
190.0000
170.0000
170.0000
180.0000-
180.0000
180.0000
130.0000
170.0000
170.0000
170.0000
170.0000
170.0000
170.0000
165.0000
175.0000
170.0000
170.0000
175.0000
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190.0000
9400.0000
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9600.0000
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9700.0000
10000.0000
10100.0000
10100.0000
10000.0000
10000.0000 	
10500.0000
10400.0000
10100.0000
10100.0000
10000.0000
10200.0000 -
10200.0000
10200.0000
10200.0000
10200.0000
10200.0000
MISSING
MISSING
MISSING
MISSING
MISSING
MISSING
MISSIN&
MISSING
MISSING
MISSING
MISSING
MISSING
MISSING
MISSING
MISSING
MISSING
-ISSING
"ISSING
-ISSING
MISSING
MISSING
MISSING
"ISSING
"ISSING
8 PAN AMPS
230.0000
220.0000 	
220.0000
230.0000
260.0000
280.0000
280.0000
230.0000
250.0000
220.0000
230.0000-
250.0000
250.0000
250iOOOO 	
170.0000
200.0000
220.0000 	
220.0000
240.0000
2*&cOO
-------
to
vo
SE NO.
130
181
182
183
184
185
186
187
188
189
190
191
192
193
194
195
196
197
198
* AA —
199
200
201
202
203
204
205
206
207
208
209
210
211
213
313
214
215
216
217
218
219
220
231
222
223
334
225
236
227
228
239
230
231
232
333
?34
2J5
236
237
238
239
240
1 S03INPPM
1300.0000
1080.-0000
1080.0000
loec.oooo
1080.0000
1140.0000
1080.0000
1080.0000
1080.0000
1140.0000
1140.0000
1140.0000
1140.0000
1080.0000-
1140.0000
1080.0000
1020.0000
1020.0000
1140.0000
1140.0000-
1140.0000
1140.0000
1140.0000
1140.0000
1140.0000
1140.0000
1140.0000
1140.0000
1140.0000
1080.0000
1080.0000
1080.0000
1020.0000
1020.0000
960.0000
960.0000
960.0000
1020.0000
1030.0000
1030.0000
1020.0000
1200.0000
1020.0000
1110.0000
1080.0000
1080.0000
1080.0000
1140.0000
ineo.oooo
1140.0000
1140.0000
1140.0000
1140.0000
1140.0000
1140.0000
1140.0000
"40.0000
1080.0000
1140.0000
1140.0000
1080.0000
2 sso2 BEM
a*..ooor
78.8900
78.8900
78.8900
78.3300
83.1100
77.7800
77.7800
77.7800
76.3200
7^.6600
71.6800
71.6800
75.5600" •
77.8900
76.1100
74.7100
74.7100
77.8900
W %7 i% A-
7 T.370O
76.3200
76.3200
77.3700
76.3200
74.7400
76.3200
7f .3200
76.3200
7*. 3200
75.5600
7*. 6700
76.6700
7«-.4700
76.4700
72.5000
75.6300
75.6300
79.4100
76.4700
76.4700
76.4700
MISSING
30.5900
83.7800
77.7800
82.7800
74.3300
83.6800
hi .6700
82.6300
76.3200
7«.3300
7*. 3300
7*. 3200
7*.3?00
7«..320P
7-5.0000
81.6700
73.9500
7«.950P
77.7800
3 PH
7.0000
6.9000-
6.7000
6.9000
6.9000
7.0000
7.1000
6.9000
6.9000
6.7000
6.7000
7.0000
7.0000
-7.0000
6.9000
7.0000
7.0000
7.1000
7.0000
7.0000"-
7.1000
7.0000
7.0000
7.0000
7.1000
7.0000-
6.9000
7.0000
7.0000
7.0000
7.1000
7.1000
7.1000
7.1000
7.1000
7.3000
7.3000
7.2000
7.0000
7.0000
7.0000
7.5000
7.1000
7.1000
7.1000
7.1000
7.0000
7.0000
7.1000
7.1000
7.0000
7.1000
7.1000
7.2000
7.2000
7.3000
7.3000
7.1000
7.0000
7.1000
7.0000
4 DELTA P
4.0000
	 4.0DOO —
5.1000
3.9000
6.0000
8.0000
5.8000
7.0000
7.0000
6.0000
6.0000
5.8000
S.1000
	 5.9000
6.3000
6.0000
5.5000
5.5000
6.0000
6.5000
6.4000
7.0000
6.8000
6.6000
MISSING
~ 6.600 0
6.5000
6.5000
6.5000
6.5000
6.5000
6.5000
6.6000
6.2000
5.4000
3.0000
3.0000
5.5000
5.3000
5.2000
5.2000
6.6000
8.0000
9.5000
9.5000
9.0000
8.4000
8.4QOO
8.4000
8.5000
9.0000
9.0000
9.0000
9.onoo
9.0000
9.0000
7.0000
8.4000
8.5000
6.5000
8.5000
> D OAS T
315.0000
300.0000
400.0000
345.0000
335.0000
335.0000
400.0000
340.0000
340.0000
280.0000
380.0000
365. GOOD
410.0000
420".00«0-
420.0000
435.0000
425.0000
450.0000
450.0000
- 450.000t>"- "
430.0000
410.0000
390.0000
365.0000
370.0000
360.0000-
360.0000
350.0000
350.0000
350.0000
330.0000
350.0000
340.0000
350.0000
375.0000
MISSING
HISSING
200.0000
250.0000
250.0000
250.0000
310.0000
225.0000
225.0000
225.0000
275.0000
280.0000
275.0000
270.0000
285.0000
270.0000
260.0000
260.0000
250.0000
350.0000
?50.0000
280.0000
310.0000
290.COOO
275. "000
300.0000
6 0 PROD T
180.0000
165.0000 —
205.0000
155.0000
185.0000
180.0000
•.95.0000
160.0000
160.0000
165.0000
1*5.0000
240.0000
340.0000
25-3. OD 00 	
351.0000
263.0000
356.0000
345.0000
245.0000
260.0000
260.0000
250.0000
240.0000
335.0000
235.0000
230.0000" -
330.0000
230.0000
310.0000
310.0000
190.0000
190.0000
200.0000
300.0000
250.0000
MISSING
MISSING
MISSING
185.0000
185.0000
185.0000
195.0000
170.0000
180.0000
210.0000
310.0000
210.0000
205.0000
210.0000
210.0000
200.0000
190.0000
190.0000
190.0000
190.0000
190.0000
295.0000
210.0000
190.0000
?00.0000
210.0000
7 CIPC GPM
MISSING
*!lSSI*iG —
MISSING
MISSING
MISSING
MISSING
MISSING
MISSING
MISSING
MISSING
MISSING
MISSING
MISSING
- -MISSING —
MISSING
HISSING
MISSING
MISSING
HISSING
MISSING
HISSING
HISSING
HISSING
MISSING
MISSING
KISSING
MISSING
MISSING
MISSING
MISSING
MISSING
MISSING
MISSING
MISSING
MISSING
MISSING
MISSING
MISSING
MISSING
HISSING
MISSING
HISSING
MISSING
MISSING
MISSING
MISSING
MISSING
HISSING
MISSING
MISSING
MISSING
MISSING
MISSING
MISSING
MISSING
MISSING
MISSING
MISSING
MISSING
MISSING
-ISSING
8 FAN AMPS
190.0000
190.0000- ~
1EO.COOO
170.0000
210.0000
230.0000
300.0000
330.0000---
190.0000
300.0000
200.0000
200.0000
300.0000
--208TOOOO- —
200.0000
200.0000
200.0000
200.0000
210.0000
21 0.0000
210.0000
210.0000
210.0000-
310.0000
210.0000
-210-.0000-- -
210.0000
210.0000
210.0000
210.0000
210.0000
210.0000 —
210.0000
210.0000
210.0000
170.0000
200.0000
200.0000
200.0000
200.0000
200.0000
210.0000
230.0000
240.0000-
240.0000
240.0000
230.0000
240.0000
240.0000
240.0000
240.0000
240.0000
240.0000
240.0000
240.0000
240.0000
240.0000
240.0000
240.0000
240.0000
240.0000

-------
OJ
O
NO.
241
242
243
244
245
246
2<»7
248
249
250
251
252
253
254
255
256
25T
258
259
260
261
262
263
264
265
266
267
263
269
270
271
272
273
274
275
276
277
278
279
280
261
282
283
284
285
286
287
288
289
290
291
292
293
29»
295
296
297
298
299
300
301
1 S02IHPPM
1140.0000
1140.0000
1140.0000
MISSING
1380.0000
1140.0000
1140.0000
1230.0000
1230.0000
1080.0000
1140.0000
1?60.0000
1140.0000
1380.0000
1380.0000
1380.0600
1170.0000
' 1020.0000
1020.0000
1080. ODOO
1020.0000
1020.0000
1140.0000
1140.0000
1?00.0000
1200.0000-
1020.0000
1320.0000
1140.0000
1140.0000
1140.0000
1140.0000
1080.0000
1080.0000
1140.0000
1140.0000
1200.0000
1200.0000
1?00.0000
1200.0000
1200.0000
1080.0000
1020.0000
1080.0000
10BO.OOOO
960.0000
1020.0000
060.0000
1020.0000
1080.0000
inPO.OOOO
IOPO.OOOO
inPO.OOOO
IOHO.OOOO
1050.0000
10?0.0000
In50. 0000
IOPO.OOOO
1140.0000
inpo.oooo
1140.0000
2 5S02 REM
S?.6300
81.5800
7B.9500
MISSING
80.4300
74.7400
74.7400
79.7000
78.7000
72.2200
73.6800
76.1900
73.6800
78.2600-
78.2600
78.2600
74.3600
75.8800
7*. 8800
77.2200
74.1200
74.1200
76.3200
76.3200
7&.0000
77.0000
70.5900
77.2700
73.6800
71.6800
73.6800
73.6800
72.7800
72.2200
7->.6800
73.6800
75.0000
75.0000
80.0000
80.5000
80.5000
77.7800
76.4700
81.6700
77.7800
74.3800
81 .7600
81.250P
44.7100
8?. 8900
8?.Q90P
37.89QO
in. 3300
6?. 6100
3&.OOOP
8?. 6500
9?.ooor
80.5600
8* .?! 0*
8=>.650C
8-4.680P
3 PH
7.0000
6.8000
7.0000
7.0000
6.7000
6.9000
6.9000
7.0000
7.0000
7.0COO
7.0000
7.1000
7.1000
7.0000
7.0000
7.1000
7.1000
7.0000
6.9000
7.0000
7.1000
7.0000
6.9000
6.9000
7.1000
7.0000
6.9000
6.9000
7.1000
6.9000
7.2000
7.3000
7.3000
6.9000
7.0000
7.0000
7.0000
7.0000
7.2000
7.2000
7.2000
7.2000
7.2000
7.2000
7.2000
7.1000
6.9000
6.9COO
6.9000
7.0000
7.2000
7.3000
7.2000
7.2000
7.2000
7.0000
7.0000
6.9000
7.0000
6. "000
7.0000
1ELTA P
8.5000
8.6000-
8.5000
8.5000
7.5000
8.4000
7.4000
6.2000
4.0000
4.0000
4.0000
4.0000
4.0000
4-.4000
4.4000
4.4000
4.2000
5.0000
4.4000
5.0000 —
4.5000
4.5000
6.2000
6.2000
6.0000
6.4000
7.0000
7.0000
5.2000
4.7000
1.000
1.2000
2.8000
4.2000
4.0000
5.7000
7.2000
5.8000
5.0000
5.0000
5.0000
5.5000
4.8000
6.2000
6.2000
2.5000
6.3000
6.0000
8.0000
7.0000
7.0000
7.0000
7.0000
6.5000
6.7000
6.7000
6.7000
6.5000
6.2000
6.0000
7.0000
^ c Gis r
340.0000
305.0COO
29C. 00.00
33C.C090
32C.OOOO
275.0000
250.0000
300.0000
400.0000
410.0000
400.0000
390.0000
450.0000
390.000*
300.0000
380.0000
350.0000
325.0000
325.0000
-325.000fr
320.0000
320.0000
320.0000
330.0000
320.0000
320.0000-
320.0000
325.0000
325.0000
325.0000
325.0000
325.0000-
325.0000
335.0000
352.0000
352.0000
350.0000
350.0000
325.0000
325.0000
325.0000
325.0000
325.0000
320.0000
320.0000
318.0000
280.0000
277.0000
270.00CO
265.0000
265.0000
265.0000
265.0000
270.0000
265.0000
265.0000
280.0000
280.0000
230.P09S
260.0000
285.0000
6 D PROD T
2^0.0000
215.0000
2?5.0GOC
215.0000
210.0000
205.0000
215.0000
210.0000
185.0000
200.0000
210.0000
225.0000
225.0000
7 CIRC QPH
MISSING
- - MISSING
MI £51 VG
MJSETNG
MISSING
MISSING
MISSJNG
MISSING
MISSING
MISSING
KISSING
MISSING
MI5SING
225,-oooc — MISSING —
200.0000
175.0000
220.0000
200.0000
200.0000
MISSING
MISSING
MISSING
MISSING
MISSING
	 200.0000 — MISSING 	
205.0000
205.0000
205.0000
205.0000
200.0000
210.0000—
205.0000
218.0000
224.0000
215.0000
215.0000
215.0000
192.0000
195.0000
210.0000
215.0000
220.0000
220.0000
210.0000
210.0000
210.0000
209.0000
215.0000
220.0000
215.0000
225.0000
190.0000
197.0000
195.0000
210.0000
200.0000
200.0000
200.0000
215.0000
PDO.OOOO
195.0000
195.0000
195.0000
?15.0000
205.0000
205.0000
MISSING
MISSING
MISSING
MISSING
"ISSING
MISSING
MISSING
HISSING
MISSING
MISSING
MISSING
- MISSING
MISSING
MISSING
MISSING
MISSING
MISSING
MISSING
10200.0000
10200.0000
10200.0000
10200.0000
10200.0000
10200.0000
10200.0000
10200.0000
10200.0000
10200.0000
10200.0000
10200.0000
1020Q.OOOO
10200.0000
10200.0000
10200.0000
10200.0000
1G200.0000
10200.0000
10200.0000
10200.0000
10200.0000
10200.0000
8 FAN AMPS
240.0000
240.COOO 	
240.QQCO
24C.OCOO
2^0.0000
230.0000
210.0000
200.0000
leo.oooo
leo.oooo
1PC.OOOO
180.0000
leo.oooo
- leo^oooo —
leo.oooo
leo.oooo
leo.oooo
180.0000
leo.oooo
— leovoooo 	
190.0000
190.0000
200.0000--
200.0000
200.0000
200.0000 	
200.0000
205.0000
200.0000
190.0000
160.0000
160.0000—
170.0000
180.0000
180.0000
190.0000
200.0000
205.0000 	
190.0000
190.0000
190.0000
190.0000
190.0000
200.0000--
200.0000
150.0000
200.0000
200.0000
220.0000
210.0000
210.0000
210.0000
210.0000
210.0000
220.0000
220.0000
220.0000
220.0000
230.0000
230.0000
220.0000

-------
     CASE NO.  i SOZINPPM  z »soz PEM  3 PH
"4 DEL
5 D GAS T-  6 0 PROD T  7 CIRC GPM  8 FAN AMPS
H
I
302
303
304
305
306
307
308
309
310
311
31Z
313
314
315
316
317
318
319
320
321
322
323
324
325
326
327
328
329
330
331
332
333
334
335
336
337
336
339
340
341
342
343
344
345
346
347
3*8
3*9
350
351
352
353
354
355
356
357
358
359
360
361
362
1140.0000
1140.0000
1140.0000
1140.0000
930.0000
960.0000
"40.0000
900.0000
900.0000
900.0000
840.0000
640.0000
840.0000
840.0000
810.0000
1080.0000
940.0000
810.0000
1340.0000
900*0000
960.0000
960.0000
1020.0000
960.0000
960.0000
1080.0000
1 100.0000
1140.0000
1)40.0000
1140.0000
1700.0000
1700.0000
I'OO.OOOO
1140.0000
1 140. 0000
1080.0000
loeo.oooo
-1080.0000
1080.0000
1200.0000
1?60.0000
1320.0000
1380.0000
1?00.0000
1140.0000
1140.0000
llin.0000
1140.0000
10*0.0000
960.0000
000.0000
060.0000
1"20.0000
i •-.P.O.: ooo
IIP 1.000 3
^•1. 1000
•390.0000
390.0000
M51. 1000
1 ISC. 0000
I3po.oooo
ai.saoo
83.6800
a?. 1100
82.6300
83.8700
82.8100
82.1400
83.3300
8e.3300
8=.3300
84.2900
8*. 0000
85.0000
83.5700
77.0400
86.1100
8*. 0000
87.7800
8C.7100
8*. 3300
86.2500
86.6300
84.1200
83.7500
83.7500
84.4400
83.0900
83.6800
31.5800
31.5800
8^.0000
?.^n
"I . 11 •"*
7.0000
7.1000
7.0000
7.2000
7.3000
7.3000
7.3000
7.1000
6.9000
7.0000
7.1000
7.1000
7.2000
7.2000
7.3000
7.1000
7.1000
7.0000
7.1000
• 7.1000
7.0000
7.1000
7.0000
7.1000
7.1000
7.1000
7.0000
7.0000
7.1000
7.1000
7.00QO
7.0000
7.0000
7.0000
7.0000
7.0000
7.0COO
7.0000
7.0000
7.0000
7.1000
7. 1000
7.0000
7.0000
7.1000
7.0000
7.1000
7.0000
7.0000
7.0*00
7.1000
7.1000
7.3COO
7. isr.n
7. lor.-:
7.1000
'.1SOO
7.1)000
'.1000
T.30CO
7.0000
6.7000
6.5000
6.0000
5.5000
6.3000
6.0000
4.7000
6.0000
8.2000
8.3000
7.5000
7.0000
7.0000
7.2000
2.3000
8.0000
6.0000
9.0000
10.6000
10.4000-
12.0007)
10.000
9.8000
10.000
9.8000
10.000
9.5000
9.5000
7.5000
9.5000
9.4000
9.6000
8.4000
8.4000
3.0000
9.2000
3.2000
8.4QOO
8.4000
2.8000
6.6000
6.6000
7.0000
3.3000
3.5000
3.7000
3.5ngo
3.3COO
3. "5300
3.6000
3.60QO
3.6000
3.a?00
3. '-OP
3. ••'30
3.0-00
-.2:00
5.8-00
= .5."00
6.S'>00
*.5"00
280.0000
280.0000
MISSING
285.0000
280.0000
2AO.OOOO
305.0000
310.0000
310.0000
310.0000
300.0000
300.0000
MISSING
300.0000
300.0000
310.0000
310.0000
300.0000
280.0000
250.0000-
260.0000
260.0000
260.0000
265.0000
267.0000
272.0000
300.0000
300.0000
350.0000
350.0000
300.0000
320.0000
330.0000
320.0000
320.0000
325.0000
325.0000
335.0000
335.0000
MISSING
350.0000
370.0000
370.0000
370.0000
370.0000
385.0000
3P5.0000
380.0000
3B0.0100
385.COOO
3PO.OOOO
190.0000
»00.0000
400.0010
400.0030
4CO.On<10
410.0010
410.0000
415.0109
40-3.0000
340. ngno
200.0000
MISSING
MISSING
195.0000
192.0000
MISSING
IBS. 0000
185.0000
190.0000
203.0000
205.0000
200.0000
MISSING
200.0000
190.0000
195.0000
205.0000
210.0000
200.0000
185.0000
180.0000
180.0000
183.0000
160.~0000
175.0000
175.0000 -
165.0000
170.0000
220.0000
215.0000
190.0000
190.0000
185.0000
190.0000
185.0000
190.0000
190.0000
195.0000
192.0000
MISSING
185.0000
205.0000
230.0000
235.0000
220.0000
220.0000
?1Q.OOOO
715.0000
?1Q.OOOO
160.0000
160.0000
220.0000
?30.0000
315.0000
310.0000
305.0000
730.0000
'30.0000
'35.0000
740.0000
715.3000
10200.0000
10200.0000
10200.0000
10200.0000
MISSING
10000.0000
10500.0000
10800.0000
10800.0000
10800.0000
10400.0000
10600.0000
10600.0000
10600.0000—
HISSING
11900.0000
HISSING
11600.0000
11600.0000
11600.0000
11600.0000
11600.0000
10600.0000
10800.0000
10800.0000
10800.0000
10900.0000
10900.0000
11200.0000
11200.0000
11200.0000
11200.0000
11200.0000
11200.0000
10800.0000
1 1000.0000
11000.0000
11100.0000
11100.0000
11200.0000
11200.0000
11200.0000
11200.0000
10900.0000
10700.0000
10700.0000
10700.0000
1 1000.0000
1 1000.0000
11000.0000
I 1000.0000
1 1000.0000
11000.0000
1 1000.0000
11000.0000
10900.0000
10900.0000
1*900.0000
13900.0000
'.0900.0000
10900.0000
210.0000
210.0000 	
210.0000
210.0000
210.0000
KISSING
150.0000
200.0000
220.0000
220.0000
220.0000
220.0000
220.0000
220«000fr 	
160.0000
180.0000
200.0000
250.0000
250.0000
2so*oooa —
250.0000
250.0000
250.0000-
250.0000
250.0000
250.0000—
230.0000
230.0000
210.0000
230.0000
230.0000
230.0000
210.0000
210.0000
220.0000
220.0000
220.0000
220.0000
220.0000
170.0000
200.0000
200.0000
200.0000
160.0000
160.0000
160.0000
160.0000
160.0000
160.0000
160.0000
160.0000
160.0000
160.0000
160.0000
160.0000
160.0000
180.0000
200.0000
200.0000
200.0000
200.0000

-------
00
10
NO.
3b3
364
365
366
367
368
369
370
371
372
373
374
375
376
377
378
379
380
381
382
383
384
385
386
387
388
389
390
391
392
393
394
395
396
397
398
399
400
401
402
403
404
405
406
407
403
409
410
411
412
413
414
415
416
417
416
'1?
<>20
421
422

IC^3^"'™Dhl 3
O w t i • • ^ " ™ ™
11»C.OOOO
1140.0000
1140. OGOO
1140.0000
1140.0000
1140.0000
1140.0000
11 10.00PO
11 10.0000
ireo.oooo
1080.0000
8*0.0000
900.0000
900.0000
900.0000
900.0000
900.0000
900.0000
900.0000
f» 4-0. 0000"
840.0000
960.0000
1060.0000
loao.oooo
780.0000
760.0000
900.0000
900.0000
900.0000
000.0000
960.0000
900.0000
000.0000
900.0000
1020.0000
900.0000
son. oooo
900.0000 -
1000.0000
1140.0000
1020.0000
1120.0000
1020.0000
960.0000 —
960.0000
960.0000
1180.0000
1040.0000
1090.0000
1140.0000
000.0000
1160.0000
1*00.0000
1160.0000
ln2C.OOOO
1440.9000
144C.OOOO
l?r;.oooo
!!<•' .0000
1PCC.OOOO
!!<•<:. 0000
asos REM
£0.0000
61.5800
81.0500
8? .5800
81.5800
30.5300
31.3200
31.8900
32.160P
32.2200
8?.220n
8?. 8600
33.3300
81.3300
8*4.3300
83.3300
81.3300
81.3300
83.3300
83.5700
84.2900
80.0000
77.2200
77.2200
70.4600
7". 4600
81.3300
82.6700
88.0000
88.0000
87.5000
8*.. 6700
36.6700
86.6700
88.2400
86.6700
87.3300
87.3300
Se.6000
86.8400
87.6500
60.2400
3Q.2400
8=.0000
8=.0000
86.2500
8*. HOP
8«..7300
AT. 2200
67.3700
ofc. 6700
7?.7000
30.4000
91.3200
61.1*00
SC.P300
6*. BSD"!
87.5000
81.5100
63.510"
80.530P
3 PH
6.9COO
o.eeoe-
7.000C
7.1GOC
f.iooe
7.0000
7.2000
7.1006
7.2000
7.1000
7.0000
7.2000
7.1000
7.1000
7.1000
7.1000
7.1000
6.9000
6.9000
7.0000
7.0000
7.0000
7.0000
7.1000
7.2000
7.2000
7.2000
7.2000
7.2000
7.2000
7.1000
7.1000
7.1000
7.1000
7.1000
7.1000
7.0000
7.0000
7.0000
7.0000
7.0000
7.0000
7.1000
7.1000
7.1000
7.2000
7.1000
7.1000
7.00"0
7.0000
7.2000
7.0000
7.0000
7.0000
7.0000
7.0000
7. OGOO
7.1000
6.9000
7.1COO
7. 2000
4 DELTA P
6.5900
6.5000
6.6000
6.6COO
6.8000
6.3000
6.2000
6.5000
6.5000
6.4000
6.3000
6.3000
7.0000
7.0000
7.0000
7.0000
7.0000
8.0000
8.5000
	 8.500-0
8.8000
8.5000
4.0000
2.2000
5.9000
5.9000
5,9000
5.9000
5.9000
6.5000
8.8000
9.2000
9.2000
9.2000
9.2000
9.4000
10.3000
10.3000
9.0000
9.0000
10.000
10.000
10.000
10.000
10.000
10.000
10.2000
10.000
10.000
10.000
10.000
3.5000
3.0000
5.0000
5.0000
5.5000
6.0*100
7.0100
7.0000
7.4000
6.3000 '
5 C CAS T-
335.0000
335.0fr60-
330.0000
330.0000
330.0000
330.0000
330. OGOO
335.0000
335.0000
335.0000
335.0000
335.0000
365.0000
365.0COO
365.0000
365.0000
365.0000
360.0000
350.0000
350.0000
340.0000
330.0000
MISSING
MISSING
"ISSING
Hissr^
260.0000
260.0000
260.0000
260.0000
265.00TOO
265.0000
260.0000
260.0000
255.0000
280.0000
285.0000
285.0000
285.0000
210.0000
210.0000
210.0000
200.0000
200.0000
200.0000
200.0000
MISSING
275.0000
275.0000
275.0000
275.0000
250.0000
260.0000
MISSING
•MSSING
"ISSING
P60.0000
260.noOO
260.0000
260.0000
? nooo
6 0 PROD T
205.0000
- 2os.ooac -
250.0000
3:5.0000
2G5.000C
250.0000
21C.GOGO
215.0000
210.0000
210.0000
205.0000
180.0000
197.0000
197. MOO
197.0000
197.0000
197.0000
210.0000
220.0000
— 230.0000-
225.0000
210.0000
MISSING
MISSING
MISSING
MISSING-
185.0000
185.0000
185.0000
1 85. 0000
185.0000
185.0000
175.0000
175.0000
180.0000
170.0000
19?. 0000
192.0000
192.0000
170.0000
170.0000
170.0000
170.0000
170.0000
170.0000
170.0000
175.0000
175.0000
200.0000
200.0000
200.0000
180.0000
180.0000
MISSING
MISSING
MISSING
170.0000
180.0000
190.0000
169.0000
170.0000
7 CIRC GPM
10900.0000
1C900.0000
1 1200.0000
11200.0000
112CO.OCOO
11200. OOOD
1 1200. SOOO
11000.0000
11000.0000
11000.0000
11000.0000
11000.0000
11000.0000
H 000. 0000 	
11000.0000
11000.0000
11000.0000
10900.0000
10800.0000
10*00.0000
10800.0000
10800.0000
9900.0000
11000.0000
10900.0000
1*900.0000
10900.0000
10900.0000
10900.0000
10900.0000
11000.0000
11000.0000
11000.0000
11000.0000
11000.0000
10850.0000
10850.0000
10850.0000
10850.0000
10850.0000
10850.0000
10850.0000
11200.0000
11200. oooe
11200.0000
11200.0000
10700.0000
11050.0000
11050.0000
11050.0000
11100.0000
11400.0000
11400.0000
11400.0000
11400.0000
"ISSING
HISSING
"ISSING
11200.0000
11700.0000
11700.0000
8 FAN AMPS
200.0000
200.0000
200.0000
20C.OOOO
200.0000
2CO.OOOO
2CO.OOOO
200.0000
200.0000
200.0000
200.0000
200.0000
210.0000
2 10. -0008- ~
210.0000
210.0000
210.0000
220.0000
220.0000
220^0000 	
220.0000
220.0000
200.0000
160.0000
200.0000
200.0000—
200.0000
210.0000
220.0000
240.0000
240.0000
260.0000-
260.0000
260.0000
260.0000
260.0000
260.0000
260.0000
260.0000
260.0000
260.0000
260.0000
2fO.OOOO
260.000*--
260.0000
260.0000
260.0000
260.0000
260.0000
260.0000
260.0000
180.0000
IPO. 0000
220.0000
220.0000
220.0000
230.0000
220.0000
230.0000
230.0000
210.0000

-------
CAac NO.
424
425-
426
427
428
429
430
431
432
433
434
435
436
437
438
439
440
441
442
443-
444
445
446
447
448
449
450
451
452
453
454
455
456
457
458
459
460
461
462
463
464
465
466
467
468
469
470
471
472
473
1 auZl.'O'Ka
U40.0000
-1440.0000
1560.0000
1560.0000
1560.0000
1560.0000
1560.0000
1560.0000
1500.0000
1440.0000
1440.0000
1320.0000
1500.0000
870VOOOO-
870.0000
1020.0000
1020.0000
1060.0000
1080.0000
1020.0000
1080.0000
1140.0000
1080.0000
1200.0000
1200.0000
1200.0000
1200.0000
MISSING
1560.0000
1560.0000
1050.0000
1050.0000
1500.0000
1?00.0000
1500.0000
1500.0000
1500.0000
1380.0000
1140.0000
MISSING
1140.0000
1080.0000
1060.0000
1320.0000
1320.0000
nzo.oooo
1?60.0000
"ISSING
1140.0000
MISSING
NUMBER 3f CASES  =»EAO
-S3IJC PElH
79.4700
82.0800
82.3100
81.5400
MISSING
MISSING
MISSING
MISSING
HISSING
MISSING
MISSING
MISSING
MISSING
68.2800
68.2800
76.4700
77.0600
76.7900
76.6700
7*i7100-
75.0000
75.2600
73.3300
MISSING
MISSING
MISSING
MISSING
MISSING
MISSING
HISSING
MISSING
MISSING
82.0000
3*. 0000
94.0000
34.0000
84.4000
89.1300
38.4200
MISSING
89.4700
39.4400
39.060r
38.64QO
39.0900
89.550C
89.520"
-ISSfNG
-ISST-MG
«ISSIN5










j PH
7.
6.
7.
7.
7.
7.
7.
7.
7.
7.
7.
7.
7.
7.
7.
7.
7.
7.
7.
- 7.
7.
7.
7.
7.
7.
7.
7.
7.
7.
7.
6.
6.
7.
7.
7.
7.
7.
7.
6.
7.
7.
7.
»
1000
9000 - -
0000
1000
2000
1000
2000
1000
1000
2000
2000
1000
2000
2000
1000
2000
0000
0000
0000
oooo 	
0000
0000
1000
1000
0000
0000
1500
2000
1000
1000
9000
9000
4000
2000
1000
1000
1000
2000
9000
1000
2000
1000
MISSING
7.
7.
7.
7.
7.
7.
7.










2000
1000
1000
1000
5000
4000
4000










i/c-k f 5
6.5000
— 6-r2a»O—
6.1000
6.0000
6.0000
6.0000
6.0000
6.0000
6.2000
6.2000
6.2000
6.4000
6.0000
6.0000
6.3000
6.3000
6.8000
6.8000
6.9000
6.9000
6.9000
6.9000
7.0000
6.9000
7.0000
7. -00 00
6.5000
6.5000
3.4000
• 3.4000
1.2000
MISSING
4.5000
4.0000
4.3000
MISSING
4.4000
7.8000
3.0000
7.5000
9.0000
9.2000
9.3000
9.4QOO
9.0000
9.nnoo
B.flnoo
1.2000
10.8000
8.0000










0 GAS T" - 6 0 PROD T
260.0000
265.0000
265.0000
260.0000
263.0000
260.0000
260.0000
260.0000
265.0000
260.0000
260.0000
260.0000
260.0000
260.0000
270.0000
270.0000
285.0000
300.0000
310.0000
305.0000
305.0000
300.0000
325.0000
300.0000
310.0000
310.0000
305.0000
305.0000
MISSING
MISSING
MISSING
MISSING
MISSING
200.0000
200.0000
200.0000
200.0000
200.0000
210.0000
200.0000
210.0000
200.0000
170.0000
200.0000
200.0000
200.0000
200.0000
"ISSING
"ISSING
MISSING
170.0000
- '--170.-0000 -
190.0000
195.0000
198.0000
190.0000
188.0000
187.0000
190.0000
19?. 0000
190.0000
190.0000
190.0000
7 CIRC GPM
11900.0000
-11600.0000- -
11600.0000
11500.0000
11300.0000
11400.0000
11400.0000
11400.0000
11400.0000
11300.0000
11300.0000
11300.0000
11600.0000
8 FAN AMPS
210.0000
- -aiovoooo 	
210.0000
210.0000
210.0000
210.0000
210.0000
210.0000
210.0000
210.0000
210.0000-
210.0000
210.0000














- 145.0000—1-1000. 0000 	 ZIOrWOO 	
180.0000
180.0000
165.0000
175.0000
170.0000
— tro.oooo—
170.0000
170.0000
165.0000
174.0000
175.0000
175.0000- -
175.0000
175.0000
MISSING
MISSING
MISSING
MISSING-
MISSING
125.0000
120.0000
120.0000
125.0000
1-30.0000
155.0000
MISSING
150.0000
150.0000
145.0000
135.0000-
14Q.OOOO
135.0000
140.0000
••ISSING
MISSING
115.0000
11400.0000
11400.0000
12000.0000
11800.0000
11800.0000
i too o.oo oo- -
11800.0000
11800.0000
11800.0000
11800.0000
11800.0000
H800.0000--
11500.0000
11500.0000
11700.0000
11700.0000
11600.0000
11600.0000
11600.0000
11600.0000
11600.0000
11600.0000
11200.0000
11200.0000
11300.0000
11300.0000
11700.0000
-ISSING
MISSING
11700.0000
11700.0000
11700.0000
11700.0000
11400.0000
11400.0000
11400.0000
VARIABLE
Un UAUET UFAhl
NO.
1
2
3
4
5
6
7
a
9
S02INPPM
«S02 <»EM
PH
DELTA P
D GAS T
0 PRO^ T
CIRC RPv.
FAN AMPS
C TOROUE
I-lt *»"•
109?.
81.
7.
6.
287.
I"*.
1072C.
?lc.
37.
210.0000
210.0000
210.0000
210.0000
210.0000
-21 0-. 0000 	
210.0000
210.0000
210.0000 -
210.0000
210.0000
210.0000 	
210.0000
210.0000
190.0000 -
170.0000
160.0000
170.0000- -
200.0000
200.0000
200.0000
200.0000
200.0000
250.0000-
250.0000
240.0000
260.0000
250.0000
MISSING
240.0000 —
260.0000
260.0000
260.0000
160.0000
240.0000
240.0000
STANDARD
nC"U T ATT OM
UtV 1 A 1 I oN
136 163.471
?24 4.444
050 0.166
873 2.290
?15 57.256
475 24.719
461 911.543
PS2 28.681
770 8.549




































TOTAL
FRFOII
r rvcwu
403
382
469
466
429
432
278
468
437

-------
                9.0  LIST OF REFERENCES
 1)  Sulfuric Acid from the Stack.  Chemical Week, 197 (3)
          (1970).

 2)  Shah, I.S., Wechselblatt, P.M., Radway, J.E.  SO-
          Recovery from Smelters with Magnesium Base
          SOg Recovery Process.  AIME Environmental
          Quality Conference, Washington, D.C. (June 1971).

 3)  Shah, I.S.  Removing SO., and Acid Mist with Venturi
          Scrubbers"!  CEP^ (Hay 1971) Vol. 67, No. 5.

 4)  Kleiman, G. and Willett, H.  Relative Economics of
          Stack Gas Scrubbing US Residual Oil Desulfurization.
          API Session on Desulfurization and SO, Recovery
          San Francisco, Calif., (May 12, 1971)7

 5)  Shah, I.S., Quigley, C.P.  Magnesium Base SOp Recovery
          Process, A Prototype Installation.70tR AIChE
          National Meeting, (August 1971).

 6)  Wechselblatt, P.M., Quig, R.H.  Magnesium Base S02
          Recovery Scrubbing Systems.71st AIChE National
          Meeting, (February 1972).

 7)  Maxwell, M.A., Koehler,  G.R.  The Magnesia Slurry SOp
          Recovery Process with a Large Prototype System.
          65th AIChE Annual Meeting, (November 1972).

 8)  Quigley, C.P.  Progress Report - Magnesium Oxide System
          at Boston Edison Company's Mystic Station.
          Electrical Worlds Technical Conference, Chicago,
          (October 1972) .

 9)  Houston, P. and Koehler, G.  Application of Magnesia
          SO- Control System to a 150 MW Power Plant.
          International Conference on S02 Control,
          Manchester, England (April 1973).

10)  Koehler, G.R. (Part I) and Quigley, C.P. (Part II)
          Operational Performance of the Chemico Basic
          Magnesium Oxide System at the Boston Edison
          Company Flue Gas Desulfurization Symposium.
          New Orleans,  (May 1973).  (EPA-650/2-73-038,
          December 1973) .
                       - 134 -

-------
11)   Radway,  J.E.  and Rohrbach,  R.R.   Progress Report on
        the Chemico-Basic Magnesium Oxide Flue Gas
        Desulfurization System at the Boston Edison
        Company.   Presented at the 30th Annual Meeting,
        East Central Section APCA, Cleveland, Ohio
        (September 26, 1973).

12)   Maxwell, M.A.  Application of the Magnesia Slurry SO^
        Recovery Process to Stack Gas Desulfurization.
        Paper presented at 25th Southeastern Regional
        Meeting,  American Chemical Society, Charleston,  S.C.
        (November 8, 1973).

13)   Koehler, G.R.  New England S02 Recovery Project -
        System Performance.66th AlChE Annual Meeting,
        Philadelphia  (November 1973).

14)   Koehler, G.R.  Alkaline Scrubbing Removes Sulfur
        Dioxide.   Chemical Engineering Progress, 70, No. 6
        74.

15)   Koehler, G.R. and Dober, E.  Magnesia SOg Absorption
        Process Development.  Flue Gas Desulfurization
        Symposium, Atlanta, Ga.    (November 1974)
        (EPA-650/2-74-126) .

16)   Quigley, C.P. and Burns, J.A.  Assessment of Prototype
        Operation and Future Expansion Study - Magnesia
        Scrubbing Mystic Generating Station Boston,
        Massachusetts (Ibid).

17)   Erdman,  D.A.   Mag-Ox Scrubbing Experience at the Coal-
        Fired Dickerson Station, Potomac Electric Power
        Company"Washington, D.C.(Ibid).

18)   Zonis, I.S.,  Olmsted, F., Hoist, K.A. and Cunningham,
        D.M.   The Production and Marketing of Sulfuric
        Acid From the Magnesium Oxide Flue Gas Desulfurization
        Process"!   (Ibid) .                                     "

19)-  Koehler, G.  Report of Operation of a Magnesia FGD System
        on an Oil Fired Boiler.  AIChE Symposium Series,
        No. 148,   (July 1975).
                         - 135 -

-------
20)   Koehler, G.,  Chatlynne,  C.   The Magnesia Scrubbing
        Process As Applied to an Oil-Fired Power Plant.
        EPA-600/2-75-057 (October 1975).

21)   Hess, H., Englick, J., Koehler, G.   Magnesium Oxide
        Flue Gas Desulfurization Process.  Paper presented
        at Conference on Air Quality Management in the
        Electric Power Industry, Austin,  Texas, (January 1976) .

22)  Taylor, R., Gambarani, P.,  Erdman,  D.  Summary of Operations
        of The Chemico-Basic MqO FGD System at The Pepco
        Dickerson Generating Station.  Paper presented at 1976
        EPA Symposium On Flue Gas Desulfurization, New Orleans,
        Louisiana.
                        - 136 -

-------
    10.0  CONVERSION FROM ENGLISH TO METRIC UNITS
TO CONVERT FROM
Atmosphere (normal)
Atmosphere (normal)
Barrel (42 US gallons)
British thermal unit  (BTU)
BTU/Hour
BTU/pound mass
BTU/pound mass - °F
Foot
Foot2
Foot3
Foot /minute
Foot-pound force
Gallon (US)
Gallon (US)/minute
Grain
Horsepower
Inch
Inch H20  (60°F)
Pound Force
Pound mass av
Pound mass av
                2
Pound force/inch
Pound mass/foot
°Rankine
Ton mass  (.US short)
Ton mass  (US long)
TO
Bar
Pascal
Meter3
Joule
Watt
Joules/gram
Joules/gram - K
Meter
Meter2
Meter3
Meter /minute
Joule
Meter3
Meter /hour
Milligram
Kilowatt
Centimeter
Kilopascal
Newton
Kilogram
Metric ton (tonne)
Kilopascal
Kilograms/meter
°Kelvin
Kilogram
Kilogram
MULTIPLY BY
1.01325
101,325
0.15899
1055.1
0.29307
2.32600
4.18680
0.30480
0.09290
0.02832
0.02832
1.35582
0.00379
0.22712
64.7989
0.74570
2.5400
0.24884
4.44822
0.45359
0.0004536
6.89476
16.0185
0.55556
907.185
1016.05
                       _  137 -

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                 APPENDIX I
      POST OPERATION INSPECTION REPORT
      DATE OF INSPECTION - Jan. 17-24, 1975
(NOTE:  Refer to Figure 1-1, where numbers refer to follow-
ing sections)

Plumb Bob Control Mechanism
Operation has been satisfactory.
Upper Section of 1st Stage (5)
(a)  The polyester coating was gone from the stem and the
     top 8" of sloping sides of the plumb bob.  The metal
     is type 316L stainless steel at this point and measure-
     ments indicated no loss of thickness.
(b)  The coating was also gone from most of the 316 stain-
     less steel lip projecting from the sloping wall just
     above the throat.
(c)  In the throat area there were about 10 spots ranging
     in size from 12 square inches to 30 square inches
     where the entire coating had been removed from the
     metal.  The metal is 316L stainless steel at this point.
     It is possible that these coating failures were caused,
     by debris from the 4 inch stainless steel nozzles
     which had failed.
(d)  Above the projecting lip on the sloping outer wall,
     there were a number of holes in the lining where the
     carbon steel had been attacked so that only the lining
     on the other side of the steel plate prevented a hole
     in the vessel.  The figure is typical of this type of
     failure.
                      -  138  -

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        OOTUMft
FIGURE I- I
    - 139 -

-------
 (e)  As was discussed previously in the section on corro-
     sion of stainless steel all of the 4-inch tangential
     nozzles were subjected to extensive failure.  Two
     were still in place, but were in shreds.
 (f)  The three six-inch stainless steel lines that feed the
     center manifold were subjected to the same type of
     attack as the four-inch tangential nozzles and pipes.
     There was less severity because of the protective
     coating of brick cast which had been applied over these
     pipes.  Repairs have been carried out by removing the
     brick cast and coating these six-inch pipes with glass
     reinforced polyester plastic.
 (g)  The center manifold was in good condition both inter-
     nally and externally.
 (h)  There were two holes through the external wall of the
     vessel adjacent to tangential inlet nozzles.  It is
     not known the extent to which these were caused by nor-
     mal erosion or by impaction by partially failed inlet
     nozzles.  Except for these two failures the coating at
     this portion of the vessel was in good condition.
Lower Section of 1st Stage  /g^
 (a)  The polyester lining was in fair condition, with re-
     pairs needed at several points in the throat section,
     at the bottom of the skirt and on the outer surface
     of the inner skirt.
 (b)  There was one small (3/8 inch diameter)  hole in the
     bottom of the cone near the vortex breaker where a
     repair had been made.
                     - 140 -

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 (c)  There was considerable loss of metal by corrosion of
     type 316 stainless steel from the hanger rods, clips,
     clamps and bolts.  As indicated previously, corrosion
     was most severe in areas which had been stressed and
     the replacement pieces have been stress-relieved before
     installation.
1st Stage Mist Eliminator Section  (?)
 (a)  The mist eliminators were clean and in excellent con-
     dition.  However, all of the J hooks and clips used
     as hold-downs had failed and most were completely mis-
     sing.  These are among the sources of metal that have
     contributed to failures of rubber-lined pipe.  The 2
     inch x 0.2 inch straps used as auxiliary hold-downs
     for the mist eliminators have performed their function
     well.  There is evidence of slight pitting, but no loss
     of thickness.
 (b)  The new clevis type 1st stage cone support hangers
     showed slight signs of pitting, but are structurally
     in excellent condition.  These were of 316 stainless
     steel and were installed in July 1974.  The Inconel
     625 pins installed with them were in excellent condi-
     tion and showed no sign of attack.
 (c)  The 1st stage mist eliminator wash system has operated
     satisfactorily.
Upper Section of 2nd Stage  (8)
This portion of the scrubber was found to be in generally
good condition.  There was a small hole (possibly 1/16
inch in diameter) in the stainless steel pipe just below the
base.
                       -  141  -

-------
Inspection Report (Information of two-stage scrubber
absorber and the recycle pipe have been presented in
the previous report).
2nd Stage Throat Area   (9)
Failure of the coating in the area of the 2nd stage throat
was very extensive as illustrated in photographs 10-7 and
10-10.  Assurance of adequate structural integrity was pro-
vided by a series of thickness measurements.

The throat restrictor provided substantial protection for
the inner surface of the throat except where there apparently
were gaps between the restrictor and the inner surface.
Planned repairs and changes include division into an inner
and outer ring, a reduction in the total width (to decrease
pressure drop), and caulking between the restrictor plates
and walls to eliminate flow and erosion at these points.
Gas Systems
(1)  Fan
     The fan has given excellent service throughout the
     entire history of the scrubber.  Inspection indicated
     that the rotor, which is of high alloy stainless steel
     is in a condition apparently as good as new.  The
     rubber lining of the fan housing is also in a condition
     as good as new.  The only problem was a failure in one
     of the pipes which feeds water to the fan rotor.  This
     pipe had failed presumably as a result of continued
     vibration.  Repairs were effected by welding.
(2)  Secondary Mist Eliminator
     The secondary mist eliminator was clean and in excel-
     lent condition except for some evidences of corrosion
     of the various 316 stainless steel hanger rods, etc.
     This was similar to the corrosion observed in the 1st
     stage of the scrubber although substantially less in
     extent.
                      - 142 -

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(3)  Ducts and Dampers
     There was a fair amount of build-up of fly ash in the
     ducts as would be expected, but the ducts were other-
     wise in good condition.  The major problem with the
     dampers has been leakage during shut down, permitting
     a flow of gas backwards through the ducts and scrubber
     and a progressive increase in fly ash build-up and de-
     crease in damper effectiveness.  At the conclusion of
     operations in late January, whenever the scrubber was
     shut down there was a very high flow of gas backwards
     through the scrubber.
     A seal ring has now been installed on the outlet dam-
     per, with the expectation of drastically reducing (and
     possibly eliminating) this problem.  It is also expected
     that better continuity of operation will be obtained
     and this in itself will permit better performance of
     the dampers on the few occasions when shut downs are
     expected to be necessary.
Liquid Systems
(1)  1st Stage Recycle Pumps
     These have performed excellently at all times.  In-
     spection through the suction piping indicates an
     appearance "like new."
(2)  Thickeners
     These have performed satisfactorily.  The south
     thickener had a number of failures in the coating
     which were repaired.  The north thickener, in contrast,
     had no coating failures.  The bolts that hold the arms
     of the thickener rakes were corroded excessively in the
     south thickener, but little or no corrosion was observed
     in the similar bolts in the north thickener.
                    - 143 -

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(3)  Thickener Underflow System
    This system has performed satisfactorily and  inspec-
    tion did not indicate any defects.
(4)  Thickener Overflow Return System
    This system has performed satisfactorily from a
    mechanical standpoint and inspection did not  indicate
    any defects.
(5)  2nd Stage Recycle Pumps
    These pumps have given generally satisfactory perfor-
    mance.   The impeller on  each of  the  three pumps  has
    been replaced once.   In  a commercial installation it
    is  expected that rubber  covered  impellers would  be
    specified and that impeller replacement  would not be
    necessary.  At the conclusion of the operating period
    in  late January 1975,  performance curves were obtained
    on  the three pumps as indicated  in Figure 1-2.
(6)  Mother Liquor Tank
    This tank has given satisfactory performance. The
    gears on the agitator were replaced  on one occasion.
    Presumably their failure was due to  a build up of
    solids in the bottom of  the tank leading to excessive
    side thrusts on the agitator.
(7)  Mother Liquor Pumps
    Operation has been satisfactory.
(8)  MgO Premix Tank
    Operation of this tank has been  satisfactory  since
    the changes were made in the summer  of 1974.
                        -  144  -

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                          FIGURE 1-2
9000 _.
        PERFORMANCE  CURVES
      2nd  STAGE RECYCLE PUMPS
8000 __
7000 --
6000 --
          Scrubber Level 24%
            January 1975
5000 __
         S
         8
4000  __
3000 --
2000
1000  __
-0-  "A"  Pump
-D-  »B"  Pump


-A-  "c"  Pump
                                 PSI
               To        Jo       30
                              '40
50
70
                                     - 145 -

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(9)  MgO Slurry Tank
     Operation has been satisfactory except that the steam
     sparger has plugged repeatedly.  During the current
     boiler outage, the location of the steam inlet line
     has been changed.  The line now enters through the
     top of the tank and is so arranged that the sparger
     may be unplugged if plugging should continue.  It will
     also be possible to change to other sparger designs if
     such becomes necessary in order to eliminate plugging.
(10)  MgO Slurry Feed Pumps
     Operation has been satisfactory since October 1974,
     at which time a larger pump was installed as the east
     MgO pump.  One remaining problem with this system is
     that it is necessary to operate both pumps in order to
     obtain correct reading of the temperature control ele-
     ment.  A change in the location of this element is
     planned so that the operation may be carried out with
     only one pump, reserving the other as a spare.
Solids Systems
(1)  MgO Unloading
     This system has operated satisfactorily in all respects
     except that a leak developed in the elbow at the top of
     the loading line, as was to be expected.  Repairs were
     made by welding which will be adequate for the remain-
     ing three months of expected operation of this system.
     For a commercial installation materials more resistant
     to erosion would be specified for the elbows in unload-
     ing lines.
(2)  MgO Storage Bin
     Operation has been satisfactory.
(3)  MgO Weigh Feeder
     Operation of this system has been acceptable since
                      -  146  -

-------
     changes  were  made  in  the  summer  of  1974.   However,
     the reliability  of this system leaves  something  to
     be  desired  and for future commerical installations,
     other designs would be investigated.   There have
     been several  belt  failures during the  operation  of
     this system.  Near the end of operation  in late
     January,  the  weigh feeder became most  unreliable in
     its operation and  during  the outage, moderately  ex-
     tensive  repairs  and replacements have  been carried
     out.
(4)   Centrifuge
     Operation of  the centrifuge has  been generally quite
     satisfactory  and very substantially improved  over
     operation experienced at  Boston  Edison Company.   A
     major difference between  the two installations,  of
     course,  is  that  at Boston Edison the centrifuge  feed
     contained primarily magnesium sulfite  trihydrate where-
     as  at PEPCO the  feed  has  been primarily  magnesium sul-
     fite hexahydrate.   There  are four areas  that  require
     comment:
     (a)   There  has been no evidence  of  the type of binding
          between  the conveyor and the bowl (internally)
          that was so troublesome at  Boston Edison.   Rota-
          tion of  the centrifuge was  continued  most of the
          time,  although there were substantial periods
          when the machine was shut down and  binding  might
          have taken  place.  The washing procedures deve-
          loped  at Boston  Edison were applied at PEPCO from
          the start of  the operations.   The extent of inter-
          nal wear, which  is probably directly  related to
          binding, could not be determined.   The desirability
                      - 147 -

-------
     of dismantling the centrifuge for inspection
     was recognized,  but when weighed against the
     cost involved, the decision was made to resume
     operations without inspection of the internal
     portions of the  centrifuge.
(b)   There was excessive erosion-corrosion of the
     case at the liquid end,  as shown in photograph
     3-2.   A patch was applied around the entire 180°
     circumference of the casing.   Wear continued and
     the casing, which was originally 1/4 inch thick,
     was worn through completely,  exposing the patch
     for a longitudinal distance of about 1-1/2 inches.
     Although replacement patching internally with
     stainless steel  would probably have provided a
     permanent cure to this erosion problem, the deci-
     sion was made, in the interest of economy, to
     patch the casing with carbon steel.   A coupon of
     316 stainless steel has  been installed and obser-
     vation will be made at the conclusion of the operat-
     ing period as to the ability of type 316 to with-
     stand this service.
(c)   One plow failed  and all  of the plows were replaced
     in September 1974.  One  plow from the new set
     failed in January 1975 and a complete third set of
     plows has now been installed.   An improved design
     of plow may be expected  to eliminate this problem
     in future installations.   The photographs 3-5 (the
     failed plow)  and 3-11 (normal plows)  suggest that
     some machines are designed with three bolts per
     plow.
                 - 148 -

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(5)   Screw Conveyors
     These have given generally satisfactory performance.
     There is,  of course,  considerable  evidence  of  wear,
     but it is  not regarded as excessive.   The bearing  at
     the inboard end of  the dryer  feed  screw was dislodged
     due to a spreading  of the bearing  support as illustra-
     ted in photograph 4-3.  The screw  continued to operate
     without any inboard bearing,  using the solids  in the
     trough as  support,  for several  weeks.   This bearing has
     now been replaced.
(6)   Dryer
     The dryer  has given excellent performance.   Buildup
     has been limited in amount and  it  has  been  possible
     to clean the dryer  usually by an adjustment in operat-
     ing conditions, although occasionally  it has been  neces-
     sary to use a pipe  or rod for this purpose. At the con-
     clusion of operations in late January, the  dryer was
     remarkably clean, as  illustrated in photograph 4-1.
     The refractory of the burner  block and the  metal casing
     around it  failed as indicated in photograph 4-6 and
     have been  replaced.
(7)   Dryer Off-Gas Cyclone
     The double gate at  the base of  this cyclone has never
     operated properly and a rotary  valve has now been  in-
     stalled to replace  it.  In the  past, failure to remove
     solids from the base  of the cyclone has led to an  ex-
     cessive carry-over  of fines and recycle to  the scrubber.
     This situation should be substantially improved as a
     result of  the installation of the  rotary dust  valve.
(8)   Dryer Off-Gas Fan
     Operation  has been  satisfactory.
                    - 149 -

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(9)   Bucket Elevator
     It appears that the bucket elevator was sized for a
     product of higher density and possibly sized in ex-
     pectation of continuous operation at a uniform rate.
     In any event,  the capacity of the bucket elevator has
     been inadequate to handle the full load of  the scrub-
     ber system and has made it necessary to operate at rates
     approximating 75% of gas flow capacity and  somewhat
     less than 75% of magnesium sulfite capacity.   Larger
     buckets have now been installed  on the bucket elevator
     and it is expected that capacity operation  can be
     achieved at this point in the system as well as else-
     where.
(10)  Magnesium Sulfite Storage Silo
     Operation has been satisfactory.
(11)  Magnesium Sulfite Loading System
     Mechanical operation of this  system is considered
     satisfactory.   The repeated problems that have been
     experienced with excessive spillage of magnesium sulfite
     during loading are considered due to operating problems
     rather than to defects in the mechanical design or
     condition of the equipment.
                    - 150 -

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2 o ^RS
                                     151

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10-7
                                              152

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              APPENDIX 2




SULFUR OXIDE REMOVAL FROM POWER PLANT STACK GAS

   Magnesia Scrubbing-Regeneration:   Production of Sulfuric Acid
   The Thermal Dehydration of Magnesium Sulfite
   Hexahydrate (MgSO.'6H20) and Magnesium Sulfite
   Trihydrate (MgS03-3H20);

   A mechanistic Study using Thermo-analytical
   Techniques and the Development of an Analytical
   Method for Quantitating Mixtures of the Hydrates
       by

   Prof. Leonard Dauerman
   Department of Chemical Engineering and Chemistry
   New Jersey Institute of Technology
   Newark,  New Jersey
       Prepared for

   Chemical Construction Co.
   New York, New York
   February, 1975

              -  153 -

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                           ABSTRACT



     The thermal dehydration of MgS(>3.3H20 and MgS03.6H20 have been



studied by differential thermal analysis, differential scanning



calorimetry and thermal gravimetric analysis.



     Similar studies by other groups led to contradictory conclu-



sions.  In this investigation, these results were reconciled and



it was concluded that MgS(>3.6H20, under equilibrium conditions,



dehydrates in two steps through the intermediate formation of



MgS03.3H20.



     One consequence of this work is the development of a simple



analytical procedure, using TGA, for the quantitative determination



of both hydrates in mixtures and in the presence of thermally in-



active material.
                          - 154 -

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                  TABLE OF CONTENTS





ABSTRACT                                         154




TABLE OF CONTENTS                                155




LIST OF TABLES                                   156




LIST OF FIGURES                                  157




INTRODUCTION                                     158




EXPERIMENTAL                                     161




RESULTS AND DISCUSSION                           163




APPLICATION                                      168




REFERENCES                                       172



TABLES 1-6 inclusive                             173-178




FIGURES 1-22 inclusive                           179-200
                         - 155 -

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                     LIST OF TABLES
No.                                                Page
1. Starting Temperature of Thermal Dehydration     17.3
   of MgS03.3H2Q
2. Starting Temperature of Thermal Dehydration     174
   of MgS03.6H20
3. Calculated and Observed Values of Water         175
   Content in Synthetic Mixtures
*. M8SO,.3H 0 Content from TGA                     176
       3   2
5. MgS03.6H20 Content from TGA
6. TGA Results of a Synthetic Mixture
   Containing Thermally Inactive .'Mre
                         - 156 -

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                     LIST OF FIGURES
No.                                                   Page
1  DTA of MgS03.3H20                                   179
2  DTA of MgS03.6H20                                   18-°
3  DSC of MgS03.3H20                                   181
H  DSC of MgS03.6H20                                   18.2
5  TGA of MgSO .3H20                                   183
6  TGA of MgS03.6H20                                   184
7  TGA of MgS03.3H_0 under self-generated atmosphere    18^5
8  TGA of MgS036H20 under self-generated atmosphere     186
9  TGA of Std #1                                       187
10 TGA of Std #2                                       1S8
11 TGA of Std #3                                       1£9
12 TGA of Std #U                                       19-°
13 TGA of Std #5                                       191
W TGA of Std #6                                       192
15 TGA of Std #7                                       193
16 TGA of Std #8                                       194
17 TGA of Std #9                                       195
18 TGA of Std #10                                      196
19 TGA of Std #11                                      19,7
20 TGA of a mixture of MgS03.3H20,  MgS03.6H20 and      198
   glass beads
21 Water content versus % MgS03.3H20                   199
22 Water content versus % MgS03.GH20


                           - 157 -

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                         INTRODUCTION



      The thermal dehydration of the two known stable hydrates



of magnesium sulfite, namely, magnesium sulfite hexahydrate



(MgSG^.BHjO) and magnesium sulfite trihydrate CMgS03.3H20)



have been studied.  On the one hand, this work is of practical



importance because in the Magnesia Scrubbing Regeneration



Process (CHEMICO)^, the thermal dehydration of the magnesium



sulfite hydrates is a significant step.  On the other hand,



this study is of scientific interest because the mechanism of



the dehydration has been the subject of controversy.



      In the Magnesia Scrubbing Regeneration Process (CHEMICO),



sulfur dioxide in the flue gas is removed by scrubbing with a



magnesia (MgO) base slurry.  Hydrates of MgSOs are formed;



also MgSOij is formed by oxidation.  A portion of the slurry is



withdrawn and centrifuged.  The solid is separated from the



liquid, which is recycled.  The solids are then dehydrated in



a dryer and, afterwards, calcined at 1400°F-1600°F with coke



added to the solids.  Heating is sufficient to effect the



thermal decomposition of MgSOs; the coke reduces MgSOq. to



MgSOs.  The useful products of calcination are MgO, which is



recycled back to the slurry, and S02, which is converted to



sulfuric acid.



      Turning to the scientific relevance of this study,



thermal dehydration studies have been reported by three groups



and the results were apparently contradictory.  Okabe and








                         -  158  -

-------
Horiloused three different techniques to study the dehydration:



Differential Thermal Analysis '(DTA), X-ray and Infrared (IR).



From the DTA and X-ray results, they concluded that MgS03.6H20



loses three water molecules between 60°C and 100°C to form



MgS03.3H20.  The latter at 200°C completely dehydrates to



yield amorphus anhydrous MgS03.  But in the infrared investi-



gation, they reported that the spectra does not change when



the trihydrate goes to the anhydrous state at 200°C.  It does



not seem plausible that the transformation suggested could



have  occurred without any change in the infrared spectra.



The band in the 3500 cm   region is obviously an 0-H stretching



band, therefore, if the salt is dehydrated it would be expected



that this band would disappear.



      Two other investigations using DTA were carried out by



groups at the Tennessee Valley Authority (TVA).  These studies



were not published, but are presented, in part, in an EPA-



sponsored critical analysis of the Magnesia Process prepared



by TVA *•"•'.  In the above cited report, Jordan's work based upon



DTA leads to the conclusion that the thermal dehydration of



MgS03.6H20 takes place in one step starting at 100°C and that




MgS03.3H20 dehydrates in one step, starting at 160°C.



      In the other study, Hatfield and co-workers reported that



MgS03.GH20 loses nearly all its water when heated in a stream



of argon or air at 104°C for 16 hrs.  This, too, supports the



inference that the thermal dehydration of the hexa-



hydrate  occurs in one step.   It is also reported that






                          -  159 -

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     .Sj^O is partially dehydrated when heated in air for 16



hrs. at 160°C.



      In the above-cited EPA report, it is suggested that the



apparently contradictory results may be due to differences in



experimental conditions.  It was speculated that the samples



were heated in sealed tubes in the work of Okabe and Hori,



although such information was not provided in that paper.



Without presenting a critical analysis of the effects of hav-



ing the samples open or closed to the atmosphere, it is



concluded in the TVA report that the results of the TVA



groups, in which the samples are open to the atmosphere, are



valid and that MgS03.6H20 dehydrates in one step to MgS03 at



100°C.



      The purpose of this study is to reconcile the contra-



dictory results.  Thermoanalytical techniques arc used



exclusively:  Differential Thermal Analysis (DTA), Differential



Scanning Calorimetry (DSC) and Thermal Gravimetric Analysis



(TGA).  Other groups in this laboratory have studied the



thermal dehydration using Mass Spectroscopy and Infrared



Spectroscopy.  These results will be reported separately.
                          - 160 -

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                        EXPERIMENTAL



      MgS03.3H20 (97.9%) and MgS03.6H20 (99.0%) used in this



study were laboratory prepared samples.  Each hydrate was



studied individually; also synthetic mixtures of both hydrates



were studied.



      The DuPont thermal analyzer was employed in this



investigation.  This included the DuPont 900 differential



thermal analyzer (DTA) equipped with both the standard DTA



cell and the differential calorimetric cell  (DSC).  The DuPont



950 TGA unit,which is an attachment to the DuPont 900,was



also used.



      DTA (9J is a thermal technique in which the heat effects,



associated with chemical or physical changes, are recorded as



a function of temperature or time as the substance is heated at



a uniform rate.  Enthalpic changes, either-endothermic or



exothermic, are recorded.  The sample temperature is contin-



uously compared with a reference material temperature; the



difference in temperature is recorded as a function of furnace



temperature or time.  DTA is reported to have been first used



by LeChatelier'4'in 1887 for studying clay.  Since that date



many developments have been introduced and the literature has



grown exponentially.  DTA has been used for  the study of the



thermal dehydration of hydrates.  For example, the reader is



referred to the work of Wendlant and Hoiberg'  '.



      In contrast to DTA, in which the temperature difference
                           - 161  -

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between the sample and the reference is measured, in DSC it is



the heat necessary to equalize the temperature between the



sample and the reference which is measured.   This technique



thus can be used to measure enthalpic changes quantitatively.



      TGA is a technique in which a sample is continuously



weighed as it is heated at a linear rate.  The resulting



thermogram gives information concerning the thermal stability



of the substance under investigation.  TGA was first described



by Honda  ^2^in 1915.  Griffith* ^nas applied TGA to the



study of mixtures of hydrates and anhydrous salts.



      Thermal methods of analysis are uniquely applicable for



study of dehydration processes.  Dehydration can be observed



as endothermic changes in DTA, heats of dehydration in DSC,and



as weight losses in TGA.
                        - 162 -

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                   RESULTS AND DISCUSSION



     First, the DTA results will be considered.  A typical



thermogram for the 'dehydration of MgS03.3H20 is shown in



Figure 1.  Only one endothermic transition is observed, start-



ing at 190°C.  On the other hand, in the thermogram of



MgS03.6H20 shown in. Figure 2, two endothermic transitions are



observed.  One starts at 90°C and the other coinciding with



the endotherm observed for the trihydrate, starts at 190°C.



The inference to be drawn from this data is that the



hexahydrate does degrade in two steps and that the two steps



involve a transition from the hexaform to the triform.



     Next, studies were carried out using DSC.  In this case,



it is the heat input rather than the temperature which is



measured.  The DSC thermogram of MgS03.3H20 is shown in



Figure 3.  Only one endothermic transition was observed



starting at 100° C with a. peak maximum at 160° C.  Both DTA



and DSC analyses indicate that the thermal dehydration of




MgS03.3H20 is a one step process.  From DSC data, it appears



that the dehydration of MgS03.3HpO starts at a low temperature,



100°C, in contrast to the DTA data from which it is inferred



that 190°C is the starting temperature.



     The DSC thermogram of MgS03.6H20 is shown in Figure 4.



It is significant to note that only one endothermic transition



was observed starting at 45°C with a peak maximum at 90°C.



DSC results suggest that the thermal dehydration of








                        -  163  -

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takes place in one step starting at 45° C, in contrast to the



two step mechanism starting at 90°C to be drawn from the DTA



results.



     Since the phenomena measured by DTA and DSC is the same,



it was expected that the results would be consistent.



Surprisingly, this was not the case.  From the DSC data, it



appears that the dehydration of both hydrates starts at a



lower temperature and the hexaform dehydrates in one step and



not in two steps as was inferred from the DTA results.



     The apparent contradiction between the DTA and the DSC



results can be rationalized by considering the relationship



between the dehydration reaction and the sample environmental



conditions.  In any dehydration reaction water is liberated;



if the latter is continuously removed from the reaction



atmosphere two consequences are observed.  First, the



dehydration starts at a lower temperature, and, secondly,



equilibrium is not attained.



     On the one hand in the DSC studies, the sample is placed



in an open dish and is heated under a sweeping stream of



nitrogen.  Under these conditions the liberated water is



continuously removed from the reaction environment.  On the



other hand, in the DTA studies, the sample is heated in a



self-generated atmosphere because it is placed in a capillary



tube.  Under the open conditions encountered in DSC, thermal



dehydration starts at a lower temperature, t5°C versus 90°C






                              - 164 -

-------
and only one endo thermic transition is observed for the hexar
form, whereas in the HA studies two were observed.
     To confirm the above rationalization of the differences
between the DTA and the DSC studies, the thermal dehydration
was studied by another independent technique, TGA, in which
it was possible to heat the samples' either in an open
condition or in a self-generated atmosphere.  TGA thermograms,
under open conditions, were obtained by the conventional
procedure in which the sample is placed in an open platinum
dish under a sweeping blanket of nitrogen.  TGA, under self-
generated atmosphere, was achieved by placing the sample in
a capillary tube with a thermocouple inside.  Then, the whole
tube was placed in the platinum dish.
     In Figure 5, the TGA of MgS03.3H20, under open conditions
is shown.  Thermal dehydration starts at 100° C and takes place
in one step.  The weight loss of the sample is 34.0%, which
corresponds to the loss of 3 moles of water.  The effect of
operating under open conditions is shown in Figure 6  for
MgS03. 6H20.  Thermal dehydration of the hexaform starts at
70° C and takes place in one step.  The weight loss of the
sample is 51%, which corresponds to the loss of 6 moles of
water.
     The thermograms for the trihydrate and the hexahydrate,
respectively, under the conditions of a self-generated
atmosphere arc shown in Figures 7 and 8.  MgSC^.SHgO, as
                           - 165  -

-------
shown in Figure 7, loses 34.5% of its weight in one step.



This is in a very good agreement with TGA under open conditions,



but thermal dehydration starts at 220°C, i.e., at a higher



temperature, because of the self-generated atmosphere con-



ditions.  The weight loss for the hexahydrate under a self-



generated atmosphere, as shown in Fipure 8, is 51%, which



corresponds to the loss of 6 moles of water.  It is significant



to note that the thermal dehydration of the hexaform starts



at a higher temperature and takes place in two steps, with a



weight loss of 25.5% in each step.  In other words, MgS03.6H20



loses 3 moles of water in' each dehydration step.



     Thus, when the TGA study of the hexaform is carried out



under a non-equilibrium condition, because of heating the sam-



ple under a sweeping blanket of nitrogen, equilibrium is not



attained due to the continuous removal of the liberated



water.  As a result, thermal dehydration starts at a lower



temperature and takes place in one step.  On the other hand,



if equilibrium is attained, because of heating the sample in



a self-generated atmosphere, the TGA results showed that



thermal dehydration starts at a higher temperature and takes



place in two steps.  First, dehydration leads to the formation



of MgS03.3H20, then, to the anhydrous MgS03.  These TGA



observations are consistent with the explanation of the



differences observed in the DTA and the DSC studies.  The



results are summarized in Table 1 for MgS05.3H_0 and in








                            -  166  -

-------
Table 2 for MgSO .6H 0.  The onset of the endotherms as a



function of the method are compared.
                           - 167 -

-------
                        APPLICATION



     The observations made in the TGA studies were used as



bases for developing a new analytical method for quantitating



mixtures of the tri- and hexahydrates.  It had been observed



that although the second weight loss for the hexahydrate



overlapped that of the trihydrate, nevertheless, from a



knowledge of the first weight loss of the hexahydrate, the



contribution of the hexahydrate to the second weight loss



could be calculated.



     The accuracy of the method was investigated by analyzing



the thermograms of synthetic mixtures of the hexahydrate and



the trihydrate ranging from 10% to 90%.  The thermograms are



shown in Figures 9-19.



     From these thermograms, the water content and the mag-



nesium sulfite content could be calculated.  First, the water



content calculations will be considered and compared to the



theoretical values.  The water content of each hydrate in a



mixture can be obtained from the TGA thermogram, by taking



into account the fact that the weight loss in the first



dehydration step at 175°C represents the first three moles of



water in MgS03.6H20, i.e., 50% of the water content of the



hexaform.  Thus the water content can be calculated, from the



TGA thermogram, as  follows:



     % H20 in MgS03.6H20 in a mixture =  (% weight loss



               in the first step at 175°C) (2)
                             - 168  -

-------
     % H20 in MgS03.3H20 in a mixture = & weight loss in
the second step at 100° C) - (% weight loss in the first step at
                                                       175° C)
     The theoretical values of the water content are calculated
as follows:
% H20 in MgS03.6H20 in a mixture = % MgS03.6H20 in the mixture
                                   X 6H?0
                                 MgS03.6H20
                                 X 100
                                 = % MgS03.6H20 in the mixture
                                          x
                                 = % MgS03.6H20 in the mixture
                                   X 50.9
% H2Q in MgS03.3H20 in a mixture = % MgS03.3H20 in the mixture
                                     MgS03.3H20 in the mixture
                                      -   X MO
                                 = % MgS03.3H20 in the mixture
                                   X 34.1
Both theoretical and observed values of the water content are
shown in Table 3.  The percent water (observed values) is
plotted versus magnesium sulfite content in Figure 21 for
MgS03.3H20 and in Figura 22 for MgS03-6H20.
                          -  169 -

-------
     The magnesium sulfite content can be calculated from the

TGA thermograms by considering the same aspects mentioned in

the water content calculations, and, taking into account that

6 moles of water represent 50.9% by weight of MgS03.6H20,

and that 3 moles of water represent 31.1% by weight of

MgSO^.S^O.  Thus jhe percent of each hydrate in a mixture is

calculated as follows:

% MgS03.6H20 in a mixture = % weight loss at 175°C X 2 X 100
                                                         50.9

% MgS03.3H20 in a mixture =  (% weight loss between 175° and

                            «M)0°C _% weight loss at 175°C)

                            X 100
                             3TTI

The data obtained is compared versus the theoretical values in

Table 4 for the triform and in Table 5 for the hexaform.  The

accuracy of the method, as shown in Tables 4 and 5, was found

to be - 3% if no calibration curve is used.  A value of less

than 1% is to be expected if a calibration curve is used.

     Furthermore, the TGA method was tested in the presence of

TGA inactive material.  This was achieved by analyzing a

mixture of MgS03.3H20, MgSG^.eh^O and glass beads. The mixture

was subjected to the same experimental conditions of a self-

generated atmosphere.  The TGA thermogram is shown in Figure

20.  From the results summarized in Table 6, it is concluded

that this method does not suffer any interferences due to the

presence of thermally inactive materials.



                        -  170 -

-------
     Relevant to the nature of'the materials obtained in the



Magnesia Process, the quantitative analysis of mixtures of



MgSOj.SHgQ and MgS03.6H?0 has to be considered in the light



of the following contexts:  one, only these two hydrates are



present; two, in the presence of MgO, three, in the presence



of another hydrate, MgSO^.7HpO.  The latter is a common



product in the Magnesia Process.



     When only the two hydrates are present, methods available



include total sulfite by iodine titration    , X-ray



analysis     , and a wet chemical method developed by Dr. Ray



which will be referred to as Ray's Method'  '.



     In the presence of MgO and/or MgSO,.. 7^0 the measurement



of the sulfite content cannot be used to determine the ratio



of the hydrates.  From the available literature which is limit-



ed to the one paper previously cited     , it is not clear as



to whether or not quantitative analysis is possible using the



X-ray method in the presence of MgO and/or MgSO^^HjO.  Ray's



method is applicable in the presence of these materials.



     The TGA method is simpler than Ray's method but it is



not applicable in the presence of MgSO^ 7H.O.  On the other



hand, Dr. Ray*-7-' has developed a simple procedure for



quantitatively stripping MgSOg.. 71*20 from mixtures of



MgS03.3H20, MgS03.6H20 and MgO.  Therefore it appears that the



TGA technique in conjunction with Ray's stripping procedure



is the optimum method.






                       -  171 -

-------
                       REFERENCES


 (1)  Griffith,  E.J., Anal. Chem.. 29,  198  (1957)

 (2)  Honda, K.,  Sci. Rept. Tohoku Uni., 4,97  (1915)

 (3)  Karchmer,  J.H., The  Analytical Chemistry of Sulfur
     and  its  Compounds.   New  York, Wiley Interscience,
     Vol.  29, Part  I   pp  225-226  (1970)

 (4)  LeChatelier, H.,  Bull. Soc. Franc. Mineral.
     10,  203  (1887)

 (5)  Okabe, T.  and  Hori,  S.,  Tohoku University Technology
     Report.  23(2), pp 85-89  (1959)

 (6)  McGlamery,  G.G.,  Torstrick, R.L., Simpson, J.P., and
     Phillips,  J.F., Conceptual  Design and Cost Study.
     Sulfur Oxide Removal From Power  Plant Stack Gas.
     EPA-R2-73-244, pp 33-34,  (1973)

 (7)  Ray,  A.B.,  Chemical  Construction Corporation, Private
     Communication  (1974)

 (8)  Shah, I.S., Chemical Construction Corporation,  Recovery
     of Sulfur  Dioxide From Waste Gases.   U.S. 3,  577,  219
      (1971)

 (9)  Wendlant,  W.W., Thermal  Methods  of Analysis,  Second
     Edition.   New  York,  Wiley  Interscience, pp 134-201
      (1974)

(10)  Wendlant,  W.W., Hoiberg,  J.A., Anal.  Chem. Acta.
     28,  506  (1963)
                       - 172  -

-------
                          Table 1



               Starting Temperature of Thermal



                  Dehydration of MgSO?.3HgO



Technique    Experimental Conditions     Onset of the Endotherm



   DTA           self-generated                   190°C



   DSC           open conditions                  100°C



   TGA           open conditions                  100°C



   TGA           self-generated                   200° C
                        -  173 -

-------
                           Table 2



                   Starting Temperature of



              Thermal Dehydration of MgSOg.SHnO



Technique Experimental Condition First Endotherm Second Endotherm



   DTA        self-generated          90° C            190° C



   DSC        open conditions         45°C        not observed



   TGA        open conditions         70° C        not observed



   TGA        self-generated         125°C            220° C
                            -  174  -

-------
Table 3
Calculated and



of Water
Observed Values
Content in


Synthetic Mixtures


i
M
Ul
1






Stdtt
1
2
3
4
5
6
7
8
9
10
11
Composition
%MRSOP.3H,0 *MKSOo6HoO
0.0%
10.29%
18. 96%
29.37%
38.24%
50%
59.84%
70.19%
79.34%
90.18
100%
100%
84. 71%
81. 04%
70. 63%
61. 76%
50%
40. 16%
29. 81%
20.66%
9.82%
0%
Calculated 1120 content in Observed HpO content In
Triform
0%
3.5%
6.46%
10%
13.03%
17.04%
20.39%
23.91%
27.03%
30.72%
34.1%
Ilex a Form
50. 9%
45.56%
41. 19%
35.9%
31.39%
25. 42%
20. 41%
15.15%
10.5%
4.99%
0%
Total Triform
50.9%
49.06%
47.65%
45.9%
44. 42%
42.46%
40.8%
39.06%
37.53%
35.71%
34.1%
0%
3.4%
6.6%
9.0%
12%
16.4%
19.8%
23%
26.4%
30.2%
34.8%
Hexaform
52%
44.4%
39.4%
35.0%
32%
26%
20.4%
16%
10.6%
5%
0%
Total
52%
47.8%
46%
44%
44%
42.4%
40.2%
39%
37%
35.2%
34.8%

-------
Table 4
MgSOa.3H^O Content from TGA
Stdtt
1
2
3
4
5
6
7
8
9
10
11
Theoretical Value
0%
10.29%
18. 96%
29.37%
38.24%
50.0%
59.84%
70.19%
79.34%
90. 18%
100.00%
Observed Value
0%
10. 26%
19.35%
26.39%
35.24%
48.1%
58.06%
67.45%
77. 42%
88.56%
102.0%
Deviation
0%
-.03%
+.39%
-2.98%
-3.00%
-1.9%
-1. 78%
-2.74%
-1. 92%
-1.62%
+2.0%
 -  176 -

-------
Table 5


Stdft
1
2
3
4
S
6
7
8
9
10
11
MeS(h.6H,0
From
Theoretical Value
100%
89.71%
81.04%
70.63%
61.7696
50%
40.16%
29.81%
20. 66%
9.82%
0%
Content
TGA
Observed Value
102.2%
87.3%
78. 45%
68.8%
62.9%
51.11%
40.1%
31.45%
20.84%
9.83%
0%


Deviation
4-2.2%
-2.41%
-2.54%
-1.83%
+1.14%
+1.11%
-.06%
+1.64%
+.18%
+.01%
0%
- 177 -

-------
                         Table 6



                TGA results of a synthetic



               mixture containing thermally



                     inactive compound




                        Theoretical Value    Observed Value



MgS03.3H20                     W.3%             «.2#




MgS03.6H20                     30.096             29.3%



glass beads                    25.7%             27.5%*
*This value was obtained by difference
                       -  178 -

-------
                                                                         •Urt
        SAMPLE:  MgS03.3H20


           Fig. No. 1
        ORIGIN:
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       SAMPLE: MgS03.6H20
          Fig.  No.  2
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SAMPLE: N«S03.3H20


    Fig. No.  3





ORIGIN:
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SAMPLE: MgSO-.BH 0
        Fig. No.
ORIGIN:
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SAMPLE: MuS03.3H2Q
Fig. No. 5
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 80
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SAMPLE: Std #2
10.295$ MgS03.3H20
89.71% MgS03.6H20
Fig. No. 10
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-------
SAMPLE: Std #4
2'J.37% MgS03.3H20
70.03% MgS03.6H20
Fig. No. 12
SIZE. .10 mg.

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SAMPLE. Stil #5
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01.70% MgS03.6H20
Fig. No. 13
SIZE.. 12 mg.






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RUN NO. 1 DATE11/25/74
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-------
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SAMPLE: Std #6
50?5 M«S03.3H20
50% MtjS03.6H20
Fig. No. 1U
SIZE . 10 mg.





































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RUN NO. I DATEH/ZS/TU
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TIME CONSTANT 1 sec. .






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 100
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 20
                 50
100
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   TEMPERATURE*,°C
                                                                                                350
                                                                               '100
                                                                                            500
                                                                                           *»nr comii ITIOII »o« KOM iiNKmrr Of CMROMCL-UUMIL IHICMOCOUPLI*

-------
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80
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SAMPLE: Std #7
50. 8'J% MgSO .311-0
ll-0.10/o MgSO-3.611 0
Fig. No. 15
SIZE _12 mg.
















































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0 200 2SO f o 300 350 MOO M5M 501
TEMPERATURE , C • »*«.» COH«ICTIOH ton mom imt«Rir» or CH»OI«I uuuti IHIHMOCUUPK*

-------
SAMPLE: Std #8
70.19% MgS03.3H20
29.81% MgS03.6H 0
Fi«. No. 1C
SIZE 12 mg.











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-------
SAMPLH. Std #'.l
JO. 3M& MgS03.3H20
2n. r>r,% Mgso3.6ii2o
Fig. No. 17
SIZE _._.!'» mg.













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TEMPERATURE , C • »'«.» convcnM ron MM LINCMITT or CHUOMH W.UML TnCMiocourifS

-------
SAMPLE: Std #11
100?£ MRS03.3H20
Fig. No. 1«J
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-------
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SAMPLE: A mixture of:
'14.3% MgS03.r>n20
30.0% MyS03.3H20
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Fig. No. 2n
SIZE 15 m0.

















































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                                                                                        350
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                                                                                  • »»«.» COHHCCTION KM NON-llNCMir» Of CHHOMIL ALUHIl. TMf KMOCOUPHS

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90%
100%

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                               £3
                                                                                       JQUW   13 1 II (0 IKt «UI hCI   AStlU C5
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                                                                                                                                                          OQ



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                     APPENDIX 3
SULFUR OXIDE REMOVAL FROM POWER PLANT STACK GAS

   Magnesia Scrubbing-Regeneration:   Production of  Sulfuric  Acid
    A Mass Spectrometric Study of the Thermal Degradation
       of MgS03 •  3H20 and MgSO  •  6H20
    by

Prof. Leonard Dauerman
Department of Chemical Engineering and Chemistry
New Jersey Institute of Technology
Newark, New Jersey
    Prepared for

Chemical Construction Co.
New York, New York
February, 1975


                        -  201 -

-------
INTRODUCTION

          In the Magnesia process for the removal of SO. from the flue gas and
power plants, two hydrates  of magnesium sulfite - the trihydrate and the hexa-
hydrate - are formed.  At a later stage these hydrates are calcined; MgO is
formed which is recycled and, also, SO., which is converted into sulfuric acid.
          It was the aim of this study to answer several questions pertaining
to the calcining process:  How do the hydrates decompose under vacuum condi-
tions?  Are trace amounts of H_S formed in the thermal decomposition?  How
valid is the thermodynamic calculations on the partial pressure of SO. as a
function and temperature.  (K. Schwitzgebel and P. S. Lowell, "Thermodynamic
basis for existing experimental data in Mg-SO.-O. and Ca-SO.-O. systems," Env.
Sci. & Tech..7. No. 13, 1147  (Dec. 1973).
          The technique used in this study was mass spectrometry.

EXPERIMENTAL:
          Samples of the hydrates were heated in the ionization source of the
Finnigan Quadrupole 1015 mass spectrometer by utilizing the solid inlet probe.
The temperature of the solid could be heated up to 400 C and the ambient pres-
sure was approximately 10   mm.  Samples were heated to a given temperature
and spectra were taken after the spectral pattern had stabilized.
RESULTS AND DISCUSSION
          Two series of runs are presented as representative of the data obtain-
ed.  In Run //370, the spectra presented are those for the decomposition of
MgSO '3H20.  Spectra are recorded from 35  to 400 C.  The three parallel re-
cordings on each spectrum represent data recorded at three different sensitivities
                              -  202  -

-------
1:3:9.  A similar set of records for MgSO '6H_0 are presented in Run #371 series



of spectra.  As a reference record, the spectrum of SO-.H.O is shown in Figure 1.



          To determine whether or not there is a difference in the thermal de-



composition between the two hydrates, the ratios of the peak heights of  -- as
a function of temperature were calculated.



          In making these calculations data from an additional run for the tri-



hydrate, and two additional runs for the hexahydrate were used.  In Tables 1-5,



the relevant data taken from the spectra are tabulated, and the value of the



•j;-£ ratio is calculated.  In Table 6, the ratios for the three runs for MgSO-
HoO                                                                         j


• 6H70 are averaged at each temperature, and the logs are calculated.  In Table 7,



similar operations are carried out on the two MgSO '3H_0 runs.


                    SO?
          The log  CUQ) as a function of temperature for the hydrates *s plot-



ted in Figure 1.  The trend is similar.  And in the light of the precision of



the data, it can not be concluded that there is a difference in the way that the



hydrates decompose.



          Another question raised is whether H.S, even in trace amounts, is ob-



served.  The peak characteristic of H.S is observed at an m/e equal to 34.



This ra/e is observed in some spectra, for example, Run #370 at 400°C.  The ratio



of ^32/^64 is 0.00547.  In spectra Figure //I, for SO., where the intensity of



m/e 64 is of a similar value the ratio is 0.00550.  The fact that the difference



in the ratio is the within the error in measuring the intensities means that the



34 is not an independent peak due to a separate species.  It is, therefore, con-



cluded that H-S does not form even in trace amounts when the  hydrates ther-



mally decompose.



          Note that SO- is observed at very low temperatures.  In Run #370, i-fc *-s



observed at 35 C.  But the pressure is ~ 10  mm.  From Figure 2 in the previously





                                       - 203  -

-------
cited paper by Schwitzgebel and Lowell, in which the equilibrium constant is




plotted against temperature for the system MgSO,-*-SO- + MgO, it is seen that at




35°C, the predicted value of the SO. pressure is 1.2xlO~  mm.  This prediction




is consistent with the observation made in this study, therefore, it is con-




cluded that the equilibrium calculations are verified for the low temperature




region.
CONCLUSIONS






1.  Under vacuum conditions, MgSO '3H.O and MgSO3'6H_0 degrade similarly.




2.  H»S is not a thermal degradation product of the magnesium sulfite hydrates.




3.  The thermodynamic calculations for the equilibrium MgSO_-«-MgO + S02 were




    confirmed in the lower temperature region, 50-100 C.
                                   - 204  -

-------
   MASS SPECTRA OF MgSO3.6H20 & MgS03.3H2O
   RUN SERIES 370, 371,  REFERENCE MATERIAL
The numerous mass spectra taken at the temperature
intervals given in the table are not presented here
since the pertinent data have been reduced in the
subsequent tables and graphs.
                     - 205 -

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                              «
Tables 1-5.  CALCULATION OF ^£ INTENSITY RATIOS AS A
                            H20


             FUNCTION OF TEMPERATURES FOR RUNS OF VARYING



             DETECTION SENSITIVITY FOR MgS03'3H20 and



             MgS03-6H20.
                       -  206 -

-------
 Table 1.  MgSO '3H.O; Run #370; Detection Sensitivity,  1000 microamps.
Temp
35°C
50
100
150
200
250
300
350
400
64
17
8
11
13
13
28
42
110
350
m/e
18
1500
40
47
33
26
34
17
25
47
m/e
17
480
11
13
9
7
9
5
7
13
S02 64
H.O 18
0.01133
0.20
0.234
0.394
0.50
0.823
2.47
4.40
7.445
m =  atomic weight
e =  charge
                          - 207  -

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 Table 2.  MgS03'6H20; Run #371; Detection Sensitivity,  1000 Microamps
               (1)
Temp

40°C
50
100
150
200
250
300
350
400
m — f
m/e
64

36
250
250
46
86
200
440
940
3250
m/e
18

4610
15600
1830
150
180
260
260
200
350
m/e m/e
17 16

1540 90
4900 320
580 40
38
45
52
50
42
68
S02 64
H20 = 18
0.007810
0.01603
0.1366
0.307
0.478
0.769
1.692
4.70
9.286
m =  atomic weight
e =  charge
                             - 208 -

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Table 3.   MgS(>3'6H20; Run //372;  Detection Sensitivity, 500 Hicroamps.
Temp
35°C
70
150
200
250
300
350
400
64
5
24
50
33
50
98
207
423
m/e
18
450
1674
315
80
61
63
35
72
m/e
17
150
558
100
22
18
18
10
18
S02 m 64
H,0 " 18
0.0111
0.01434
0.1587
0.4125
0.8197
1.556
5.914
5.875
m =  atomic  weight
e =  charge
                           - 209 -

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    Table 4.  MgSO '3H.O;  Run //373; Detection Sensitivity, 600 Microamps,
Temp
35°C
50
100
150
200
250
300
350
400
m/e (1>
64
- -
13
10
2
2
12
20
36
113
m/e
18
16
500
350
33
32
150
140
26
42
m/e
17
5
130
80
9
8
30
28
7
11
S°2 64
H20 " 18
- -
0.026
0.0286
0.0606
0.0625
0.080
0.143
1.385
2.69
*   m =  atomic weight
   e =  charge
                             -  210 -

-------
    Table 5.  MgSO *6H20; Run #374; Detection Sensitivity, 750 Microamps.
Temp
50
100
150
200
250
300
350
400
tf(1>
13
74
160
55
88
200
520
850
m/e
18
135
4200
960
160
115
98
65
100
m/e m/e
17 J.6
45
1400 91
320
36
30
22
17
27
S02 64
H20 = 18
0.0963
0.1771
0.1667
0.3438
0.7652
2.564
8.00
8.50
'   m = atomic weight
   e = charge
                            - 211 r-

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                             SO,
     Table 6.   Ave. Ratio of H20 as a function of T (MgSO '6H 0)
Temp ( C)     Run #371
Run #372
Run #374
Ave
Log Ave
35
40
50
70
100
150
200
250
300
350
400
— —
0.007810
0.01603
—
0.1366
0.307
0.478
0.769
1.692
4.700
9.286
0.0111
—
—
0.01434
—
0.1587
0.4125
0.8197
1.556
5.914
5.875
~
—
0.0963
—
0.1771
0.1667
0.3438
0.7652
2.564
8.00
8.50
0.0111
0.007810
0.0562
0.01434
0.1569
0.2108
0.4114
0.7846
1.9373
6.205
7.887
-1.95
-2.107
-1.250
-1.843
-0.804
-0.676
-0.386
-0.105
0.287
0.793
0.897
                                 -  212  -

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                        so3
Table 7.   Ave.  Ration of H20 as a function of I (MgSO^SI^O)
Temp(°C)
35
50
100
150
200
250
300
350
400
Run #370
0.01133.
0.200
0.234
0.394
0.500
0.823
2.47
4.40
7.445
Run #373
__
0.026
0.0286
0.0606
0.0625
0.080
0.143
1.385
2.69
Ave
0.01133
0.113
0.1313
0.2273
0.2813
0.4515
1.3065
2.893
5.068
Log Ave
-1.946
-0.947
-0.8817
-0.6434
-0.5509
-0.3453
1.161
0.4612
0.7048
                        - 213 -

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                SO 9
Figure 2.   Log fc-r)     as a function of Temperature

                ««"
                 2  ave.
           for MgSO  -3H20 and
                  -  214 -

-------
      1.2
      1.0
      0.8
      0.6
      0.4
      0.2
      0
     -0.2
OJ§, -0.4 •
 O  -0.6
 O
 -J  -0.8
     -1.0
     -1.2
     -1.4
     -1.6
     -1.8
     -2.0
     -2.2
                      V  TfC)
EQUAL CONCENTRATIONS OF
  HjO AND S02
                                 QMgS03-6H20
                                 ®MgS03 3H20
      50     100
                                ISO   200   250    300   350    400
                       - 215  -

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      APPENDIX A.  Simulation of Calciner in the Laboratory; The Testing
                   of the Hypothesis that tUS is Formed When the Burner
                   Gas is Operated in the Fuel-Rich Region.
INTRODUCTION:

          Since the previous study showed that H-S is not a product of the thermal
decomposition of the magnesium sulfite hydrates, and since H_S had been reported
as a product during calcination, it was conjectured that H_S forms as a result
of reactions between SO. and hydrocarbons present when the flame used to effect
thermal degradation is operated in the fuel-rich region.
          A laboratory set-up was designed which simulates many features of a
calciner and, also, permits the immediate continuous analysis of volatilized
products.


EXPERIMENTAL:

          An inverted premix burner and a movable platform on which the sample
is situated are housed within a pyrex glass pipe.  See Figure A.  In the center
of the platform Just above the sample is a quartz probe which leads to the Fin-
nigan 1015 Quadrupole mass spectrometer.  Thus, volatiles are continuously and
rapidly characterized.  In addition, the temperature in the region is sensed by
a thermocouple.  Also, the pressure in the "cross" can be varied and controlled.
In practice, the pressure was maintained at 100 mm and the burner was operated
in the fuel-rich region.


RESULTS:

          This study was not carried out in a comprehensive manner.  In the survey-
type studies carried out, H.S was not- observed.
                                   -  216 -

-------
LAB-SCALE CALCINER SIMULATOR
              - 217 -
                              APPENDIX A

-------
          LAB-SCALE CALCINER SIMULATOR




             EXPLANATION OF NUMERALS








 1.  02 feed




 2.  Fuel feed




 3.  Premlx burner




 4.  Lead for Tejla Coil ignition




 5.  Cooling water




 6.  NaCl window




 7.  Quartz probe




 8.  Thermocouple




 9.  Perforated stainless steel cover




10.  Asbestos sheet




11.  Stainless steel sample holder




12.  Rubber stopper




13.  To mass spectrometer




14.  Position of thermal decomposition stage is adjustable




15.  To vacuum
                - 218  -

-------
      APPENDIX B.  Effect of Wettness of Hydrates on Aggregate Formation




                   During Calcining






INTRODUCTION:




          The prevalent feeling had been that less aggregation, finer particles,




resulted from the calcining of "dry"  hydrates.  On the other hand, it was thought




in this laboratory that the volatilization of water during calcination should




break up the particles.








EXPERIMENTAL:






          Samples of MgSO *3H_0 were heated in air and vacuum to 500 C.  Also,




an extra-moist sample was heated in vacuum.








RESULTS:






          Samples heated in air showed less aggregation than samples heated in




vacuum.  Extra-moistened samples heated in vacuum show less aggregation than the




drier samples.








CONCLUSION:






          Water decreases aggregation by explosive volatizatlon, thus rapid re-




moval by applying vacuum increases aggregation.  Ideally, a wet sample should be




rapidly heated to as high a temperature as possible.
                                  -  219 -

-------
                                TECHNICAL REPORT DATA
                          (Please read Instructions on the reverse before completing)
 1. REPORT NO.
 EPA-600/7-77-018
                           2.
                                                       3. RECIPIENT'S ACCESSION NO.
4. TITLE AND SUBTITLE
 Magnesia Scrubbing Applied to a Coal-Fired
    Power Plant
                                 S. REPORT DATE
                                 March 1977
                                 6. PERFORMING ORGANIZATION CODE
7. AUTHOR(S)

 George Koehler
                                                       I. PERFORMING ORGANIZATION REPORT NO.
9. PERFORMING ORGANIZATION NAME AND ADDRESS
 Chemico Air Pollution Control Company
 One Penn  Plaza
 New York, NY 10001
                                                       10. PROGRAM ELEMENT NO.
                                 EHB528
                                 11. CONTRACT/GRANT NO.
                                      68-02-1870
12. SPONSORING AGENCY NAME AND ADDRESS
 EPA, Office of Research and Development
 Industrial Environmental Research Laboratory
 Research Triangle Park, NC  27711
                                 13. TYPE OF REPORT AND PERIOD COVERED
                                 Final:  8/73-8/75	
                                 14. SPONSORING AGENCY CODE
                                  EPA-ORD
15. SUPPLEMENTARY NOTES jjjRL-RTP project officer for this report is C. J. Chatlynne, Mail
 Drop 61, 919/549-8411 Ext 2915.
i6. ABSTRACT rphe rep0rj. gjves results of a full-size demonstration of the magnesia wet-
 scrubbing system for flue gas desulfurization (FGD) on a coal-fired utility boiler. The
 system was designed to desulfurize  half the flue gas from a 190-MW rated capacity
 generating unit firing 3. 5% sulfur coal.  The FGD installation was equipped with a
 first-stage wet scrubber for particle emissions control,  followed by the magnesia
 unit.  The FGD system was able to remove 90% of the inlet SO2 over 2800 hours of
 operation logged at the generating station.  Its particle control capability was also
 demonstrated by reducing particle emissions to less than 0.01 gr/scf with the unit
 operated in series with an electrostatic precipitator.  A test  program,  using only the
 wet-scrubbing unit for particle emissions control,  achieved a collection efficiency
 of 99. 6%.  Magnesia was regenerated and recycled successfully.   The SO2 produced
 during regeneration was used to  manufacture commercial grade sulfuric acid which
 was marketed.  Correlations were developed to determine SO2 removal for varying
 boiler loads and fuel sulfur  content, and to  control regeneration of acceptable
 alkali. Several other studies of  the process technology and process chemistry were
 undertaken as part of the work.
 7.
                             KEY WORDS AND DOCUMENT ANALYSIS
                DESCRIPTORS
                                          b.lDENTIFIERS/OPEN ENDED TERMS
                                             c.  cos AT i Field/Croup
 Air Pollution
 Flue Gases
 Scrubbers
 Magnesium Oxides
 Desulfurization
 Sulfur Dioxide
Electric Power
  Plants
Coal
Combustion
Particles
Sulfuric Acid
Air Pollution Control
Stationary Sources
Magnesia Scrubbing
Particulates
13B
21B
07A
07B
07D
10B
21D
 8. DISTRIBUTION STATEMENT
 Unlimited
                                           19. SECURITY CLASS (ThisReport)
                                           Unclassified
                                             21. NO. OF PAGES
                                                 228
                    20 SECURITY CLASS (Thupage)
                     Unclassified
                                             22. PRICE
EPA Form 2220-1 (9-73)
                                         - 220  -

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