EPA-650/2-75-057-C
July 1975
Environmental Protection Technology Series
                      SURVEY OF FLUE GAS
                DESULFURIZATION  SYSTEMS
             PHILLIPS POWER STATION, DUQUESNE LIGHT CO.
                                          Ul
                                          CD

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                                  EPA-650/2-75-057-C
      SURVEY  OF  FLUE  GAS
  DESULFURIZATION  SYSTEMS
PHILLIPS  POWER STATION,  DUQUESNE LIGHT CO,
                     by

               Gerald A. Isaacs

        PEDCo-Environmental Specialists, Inc.
                   Suite 13
               Atkinson Square
             Cincinnati, Ohio 45246
          Contract No. 68-02-1321, Task 6c
              ROAP No. 21ACX-130
           Program Element No. 1AB013
        EPA Project Officer:  Norman Kaplan

            Control Systems Laboratory
       National Environmental Research Center
     Research Triangle Park, North Carolina 27711
                 Prepared for

     U.S. ENVIRONMENTAL PROTECTION AGENCY
      OFFICE OF RESEARCH AND DEVELOPMENT
            WASHINGTON,D.C. 20460

                  July 1975

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                        EPA REVIEW NOTICE

Tins report has been reviewed by tin.- National Environmental Research
Center   Research Triangle. Park, Office of Research and.Development,
EPA. and approved"'for publication.  Approval does  not signi iy^that. the
con lent;-;  necessarily-reflect the views and policies of the Environmental
Pre'eclion Agency, nor does mention of trade names or commercial
products constitute endorsement or recommendation for use.
                    RESEARCH REPORTING SERIES

Rest arch reports of the Office of Research and Development, U.S. Environ-
mental Protection Agency, have been grouped into series. These broad
categories were established to facilitate further development and applica-
tion of environmental technology.  Elimination of traditional grouping was
consciously planned to foster technology transfer and maximum interface
in related fields.  These series are:

          1.  ENVIRONMENTAL HEALTH EFFECTS RESEARCH

          2.  ENVIRONMENTAL PROTECTION TECHNOLOGY

          *  ECOLOGICAL RESEARCH

          4.  ENVIRONMENTAL MONITORING

          5.  SOCIOECONOMIC ENVIRONMENTAL STUDIES

          6.  SCIENTIFIC AND TECHNICAL ASSESSMENT REPORTS

          9.  MISCELLANEOUS

This reporl has been assigned to the ENVIRONMENTAL PROTECTION
TECHNOLOGY scries.  This series describes research performed to
develop and demonstrate instrumentation,  equipment and methodology
to repair or prevent environmental degradation from  point and non-
point sources of pollution.  This work'provides the new  or improved
technology required for the control and treatment of pollution sources
;u meet environmental quality standards.
This document is available to the public for sale through the National
Technical Information Service, Springfield, Virginia 22161.

                Publication No. EPA~650/2-75-057-c
                                 u

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                       ACKNOWLEDGMENT





     This report was prepared under the direction of Mr.



Timothy W. Devitt.  The principal author was Dr. Gerald A.



Isaacs.



     Mr. Wade H. Ponder, former EPA Project Officer, had



primary responsibility within EPA for this project report.



Information and data on plant operation were provided by Mr,



S. L. Pernick, Duquesne Light Company, and Mr. Paul Chopra,



Chemico, Inc., during and subsequent to the survey visit.




     The author appreciates the efforts and cooperation of



everyone who participated in the preparation of this report.
                              111

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                      TABLE OF CONTENTS

                                                       Page

ACKNOWLEDGMENT                                         ii

LIST OF FIGURES                                        iv

LIST OF TABLES                                         iv

SUMMARY                                                v

1.0  INTRODUCTION                                      1-1

2.0  FACILITY DESCRIPTION                              2-1

     2.1  Plant Location                               2-1

     2.2  Boiler Data                                  2-1

     2.3  Pollution Controls                           2-2

3.0  FLUE GAS DESULFURIZATION SYSTEM                   3-1

     3.1  Process Description                          3-1

     3.2  Installation Schedule                        3-7

     3.3  Cost Data                                    3-9

4.0  FGD SYSTEM PERFORMANCE ANALYSIS                   4-1

     4.1  Start-up Problems and Solutions              4-1

     4.2  Performance Test Run                         4-3

     4.3  Performance Parameters                       4-4

     4.4  Process Modification for Future              4-5
          Installations

APPENDIX A  PLANT SURVEY FORM                          A-l

APPENDIX B  PLANT PHOTOGRAPHS                          B-l

APPENDIX C  OPERATIONAL REPORTS                        'C-l

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                       LIST OF FIGURES
Figure

 3.1
General Flow Diagram of the FGD System
at the Phillips Power Station
Page

3-3
                       LIST OF TABLES
Table

 2.1



 3.1


 3.2
Data on Plant Design, Operation and
Emissions Duquesne Light Company -
Phillips Power Station

Summary of Scrubber Data - Phillips
Power Station

Summary of Tank Data - Phillips Power
Station
2-4
3-8
3-8
                              VI

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                           SUMMARY




     Four parallel Chemico venturi scrubber trains have been



installed at the 400 MW Phillips Power Station of Duquesne



Light Company.



     Each of the four trains has a first stage venturi for



S02 and particulate removal; one of the four trains includes



a second stage venturi absorber for the additional control



of S02 emissions.  The system uses slaked lime as the



absorbing medium and has been operational since July 1973.



An overall SO2 removal efficiency for the plant of 50-60



percent has been attained.  The two stage train has achieved



approximately 90 percent S02 removal efficiency.  The use of



magnesium oxide-modified lime is being investigated in an



effort to increase the S02 removal efficiency of the existing



system.




     Numerous start-up and operational problems have been



encountered and corrected.  A ten-month evaluation of the



system was initiated in December 1974 to determine whether



additional SO2 removal equipment will be installed.



     Pertinent data on the facility and FGD system operation



are summarized in the following table.
                              vn

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               SUMMARY OF FGD DATA - PHILLIPS
Station Rating

Fuel Characteristics


Prime A/E

FGD Vendor

Process

New or Retrofit

Start-up Date

FGD Modules

Efficiency, overall

     Particulate

     so2

Water Make-up

Sludge Disposal

Unit Cost
373 MW (net) after scrubber derating

Coal:  11,350 BTU/lb, 18.2% ash,
2.15% sulfur

Gibbs and Hill, Inc.

Chemico

Wet lime

Retrofit

August 1973 (SC<2 absorber)

Four first stage; one second stage



99 percent

50-60 percent

1.7 gpm/MW  (net)

Stabilization and haul to landfill

$38 million ($102/net KW) capitala

$15 million/yr  (5.9 mills/net KWH)
operating including indirect charges
on capital
  An estimated $15 million that may be required for sludge
  disposal facilities are not included in this cost.
                             Vlll

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                      1.0  INTRODUCTION





     The Control Systems  Laboratory of the U.S. Environmental



Protection Agency has initiated a study to evaluate the



performance characteristics and degree of reliability of



flue gas desulfurization  (FGD) systems on coal-fired utility



boilers in the United States.  This report on the Phillips



Power Station of Duquesne Light Company is one of a series



of reports on such systems.  It presents values of key



process design and operating parameters, describes the major



start-up and operational  problems encountered at the facility



and the measures taken to alleviate such problems, and



identifies the total installed and annualized operating



costs.



     This report is based upon information obtained during a



plant inspection on August 22, 1974, and on subsequent data



provided by Duquesne Light Company and Chemico personnel.



     Section 2.0 presents pertinent data on facility design



and operation including actual and allowable particulate and



S02 emission rates.  Section 3.0 describes the flue gas



desulfurization system and Section 4.0 analyzes FGD system



performance.
                              1-1

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                  2.0  FACILITY DESCRIPTION





2.1  PLANT LOCATION



     The Phillips Power Station of the Duquesne Light Company



is located on the Ohio River in Allegheny County, Pennsylvania,



20 miles northwest of Pittsburgh, Pennsylvania.  The area is



heavily industrialized, and the plant supplies electricity



to residential, commercial, and industrial users in Allegheny



and Beaver Counties.



2.2  BOILER DATA



     Six generating units at the station constitute a total



nominal generating capacity of 400 MW.  The net station



capacity will be 373 MW with four scrubber modules and four



absorber modules installed.  At the present time only one



absorber module has been installed.  All the generators are



cycling base load units.  Unit No. 6 is the largest generator,



having a net capacity of 143 MW.  All the boilers were



manufactured by Foster-Wheeler and are dry-bottom, pulverized-



coal-fired units.  The first unit was installed in 1942, and



the sixth one in 1956.  Coal at this station has an average,



as received, gross heating value of 11,350 BTU/lb.  Ash



content, on a dry basis, is 18.2 percent, and sulfur content



is 2.15 percent.






                              2-1

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2.3  POLLUTION CONTROLS



     Primary particulate emission control at this plant is



provided by Research-Cottrell mechanical collectors followed



by a Research-Cottrell electrostatic precipitator (ESP) on



each boiler.  The collection efficiency for this system was



originally estimated to be 90 percent.  However, disruption



of the gas flow distribution through the ESP resulted from



the design of the ducts which tie in to the FGD system so



that apparently the combined efficiency through the mechanical



and electrostatic system is only about 80 percent.



     Final particulate control is achieved by four parallel



Chemico venturi scrubbers with a design efficiency of 99



percent.  Outlet grain loadings from the scrubbers have been



measured to be less than 0.04 grains per standard cubic



foot.  These scrubbers also remove about 50 percent of the



S0_ entering them when lime is added  (for pH control).



     SO- emissions from one scrubber are further controlled



by a Chemico second-stage venturi absorber recirculating a



lime solution.  S02 removal efficiency for this two-stage



train has averaged about 90 percent based on performance



guarantee tests.  Overall SO- removal efficiency is there-



fore about 50-60 percent when pH can be maintained between



6-7.



     At the present time the FGD absorber facilities consist



of a two stage absorber module processing about 125 MW



equivalent of flue gas and three single stage absorber modules
                              2-2

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processing gas from the balance of the station's nominal 400



MW capacity.  Present plans provide for the installation of



up to three more FGD absorbers if they are found to be



necessary.



     The scrubber and absorber facilities derate the station



capacity by 14 MW.  This effects an increase in station heat



rate from a previous level of 11,500 BTU/KWH (net) to about



11,900 BTU/KWH (net).



     Table 2.1 presents pertinent data on plant design,



operation, and atmospheric emissions.
                              2-3

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              Table 2.1  DATA ON PLANT DESIGN,

                   OPERATION AND EMISSIONS

        DUQUESNE LIGHT COMPANY - PHILLIPS POWER PLANT
     Station Data
     Item
Maximum theoretical continuous generating
capacity, MW (net) with 4 scrubbers and
1 absorber operating

Average capacity factor (1974), %

Boiler manufacturer

Year placed in service

Station heat rate, BTU/KWH (net)

Maximum heat input MM BTU/hr

Stack height above grade, ft

Maximum flue gas rate, acfm @ 360°F

Emissions Controls:

     Particulates


     S02

Particulate Emission Rate:

     Allowable, Ib/MM BTU

     Actual, Ib/MM BTU

S02 Emissions Rate:

     Allowable, Ib/MM BTU

     Actual, Ib/MM BTU
      373



       70

Foster-Wheeler

1942-1957

   11,900

     4463

      340

1,850,000
Multicyclones ESP
Venturi Scrubber

Venturi Absorber
     0.08

     0.08 est



     0.6

     1.9 est
                              2-4

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            3.0  FLUE GAS DESULFURIZATION SYSTEM


3.1  PROCESS DESCRIPTION3

     Lime to be introduced to the FGD system at Phillips is

initially activated by slaking it to form calcium hydroxide.

This slaked lime, along with the recirculation calcium

sulfite-rich slurry constitute the scrubbing liquor.  Reaction

with SO2 in the flue gas takes place in the liquid phase.

Following are the principal chemical reactions in the lime-

base flue gas desulfurization processes:

     Lime slaking:  CaO + H20	*Ca(OH)2                   (1)

     Sulfite formation:  Ca(OH)2 + S02	*• CaSO- + H2O      (2)

     Bisulfite formation:  CaS03 + S02 + H20-»-Ca (HS03) 2    (3)

     Sulfate formation:  2CaS03 + 02	>• 2CaS04             (4)

Formation of sulfate (reaction 4) in the absorber module is

undesirable and should be suppressed.

     The Phillips FGD system may ultimately consists of four

identical parallel trains, each train consisting of a particulate

scrubber module and a S02 absorber module in series.  At the

present time, all six boilers have been tied in to the
  Adapted from "Duquesne Light Company, Phillips Power Station
  Lime Scrubbing Facility," Steve L. Pernick, Jr. and R. Gordon
  Knight, Presented at EPA FGD Symposium, Atlanta, November
  4-7, 1974, and supplemented with information obtained during
  plant visit.  See Appendices A and C.
                               3-1

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scrubbing system; only one of the four scrubbers has a



second-stage absorber installed in conjunction with it for



the removal of S02.  The exhaust streams of all six boilers



at the station are manifolded together so that the components



of the emission control system are not directly associated



with specific boilers.  This system allows maximum flexibility



for emission control when various components of the FGD



system must be shut down for maintenance or repair.  There



is also provision to bypass the whole FGD system under



emergency conditions.  However, in order to accomplish the



bypass it is necessary to shut down the boilers and to



remove blank-off plates from the exhaust gas stream.  Sixteen-



foot diameter ducts lead to each of the four first-stage



scrubbers.



     Figure 3.1 is a schematic flow diagram for this installa-



tion.   Hot flue gas  (about 500,000 acfm at 340°F) containing



fly ash and sulfur dioxide (about 1400 ppm SO-) enters the



first-stage scrubber and impinges upon the upper cone.  One-



half (8250 gpm) of the total scrubber recycle liquor for



each module is introduced into the vessel through the bull



nozzle where it is sprayed over the surface of the upper



cone,  to initiate the scrubber action.  The rest of the



scrubber recycle liquor enters through tangential nozzles



above the adjustable throat damper.  The flue gas and scrubbing



liquor are vigorously contacted in the throat section of the



scrubber where the particulates and some S02 are removed.
                              3-2

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GJ
I
U)
    HOT FLUE GAS  400.000cfm  340°Ft
    FROM BOILERS
      16,500 gpm.
        120°F
  1st-STAGE •
^SCRUBBER
                   COLD FLUE GAS
         DEMISTER SPRAY
                                        2nd-STAGE
                                        ABSORBER
                                                       FUEL
                                                       OIL  COMBUSTION
                                                        I      lAIR
         MAKE-UP  FROM
        OVERFLOW  PUMPS»
             BLEED TO
         ,   THICKENER
          AND CLARIFIER
            TO THICKENER TROUGH
V



sV

IBRA

 LIME
STORAGE
 SILO
                                                                        _BY_P_AS_S
                                         DEGRITTER
                                        j	r
                                                                              WEIGH
                                                                              FEEDER
                                               y^LAKER
                                             /TRANSFER
                                            **    TANK
                                                      LIME  SLAKER
                                                                                             LIME  SLURRY
                                                                                             PUMP  (2)
                         Figure  3.1.  General  flow diagram  of the  FGD system

                                     at the Phillips Power Station.

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The gas and liquor continue downward to the separator section



where, after being separated from the scrubbing liquor, the



flue gas enters a spray-washed demister where entrained



liquor is removed.  The gas leaves the scrubber and enters a



booster ID fan which is equipped with fresh water sprays to



remove any accumulation of solids resulting from scrubber



carryover.



     The ID fan housings are lined with 1/4-inch thick



natural rubber.  Wheel material is Carpenter 20 Cb 3, a



stainless steel containing niobium and tantalum.  The fan



shaft is 316L stainless steel.  Each fan is driven by a 5500



horsepower, 1200 rpm, 4160 volt electric, motor.  A closed



system supplies cooling water to the fan bearings.



     Outlet gas temperature from the first stage scrubber is



monitored and is normally in the 110-120°F range.  At 175°F



a control valve automatically opens to admit emergency



cooling water to the upper cone.  Additional temperature



rise automatically shuts down the fan and closes the isola-



tion dampers.



     The gas leaving the ID fan enters one of two vessels



depending on the train.  In the case of the three single-



stage scrubber trains, the gas enters an entrainment sepa-



rator in which entrained scrubbing liquor that has been



diluted by the fan sprays is separated and collected.  These



separators will be replaced by second-stage absorber vessels



where the test program indicates that additional absorbers



are feasible.  In the case of the S02 prototype train, gas
                              3-4

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leaving the ID fan enters a second stage absorber vessel,




which is identical in size and design to the first stage



scrubber.  This second vessel is equipped with lime slurry



injection nozzles.



     Lime is fed from a storage silo at a controlled rate to



a lime slaker where it is mixed with fresh make-up water.



The slaked lime overflows to a slaker transfer tank where



make-up water is added to provide a constant flow of lime



slurry with a 15-percent solids concentration.  Lime composi-



tion is 95 percent pure CaO, balance inert.  Design lime



requirement is 130 percent of the stoichiometric requirement.



At a station heat rate of 11,900 BTU/KWH, a coal gross heat



content of 11,350 BTU/lb and a sulfur content of 2.1 percent,



design lime consumption for the single train is calculated



to be about 4650 Ib/hr.



     The scrubbing liquor is circulated by two recycle pumps



(Carpenter 20 Cb 3).  Some of the recycle liquor is bled to



the first-stage scrubber and part of the first-stage recycle



stream is bled to the thickeners.



     Total recycle flow is about 16,500 gpm per stage with a



615 gpm bleed to the thickeners.  All single-stage vessels



have been fitted with reagent nozzles so that pH control can



be maintained and so that an approximate SO2 removal efficiency



of 50 percent can be accomplished.



     The exit gases leaving either the second stage absorber



or the entrainment separator enter a common wet duct lined



with Flakeline 103  (a product of the Ceilcote Company consisting






                              3-5

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of a glass-flake-filled modified polyester resin, subsequently
referred to as Ceilcote) which leads to a new 340 ft, acid-
resistant, brick-lined, concrete stack.  A 316L stainless
steel section of the duct, preceding the stack is equipped
with a direct oil-fired reheater unit that can raise stack
gas temperatures as much as 30°F.  Normal reheat is about
20°F.
     Bleed streams from the absorber and the scrubbers enter
a trough which feeds two 75-foot diameter thickeners.  The
overflow from these thickeners runs to an overflow tank
where it is pumped by two, 2000 gpm 316L stainless steel
pumps to the make-up line for return to the scrubber system.
     Underflow from each thickener, 105 gpm, at 40 to 45
percent solids concentration, is pumped by a 15 horsepower
pump to one of three clay-lined sludge holding ponds.  Each
pond has a capacity of about 6500 cubic yards.  Just prior
to discharge to the holding ponds, the sludge enters a
mixing tank where a stabilizing agent is added at a predetermined
rate based on the density of the sludge as it leaves the
thickener.
     Settling and curing take place in the pond.  Supernatant
liquid reenters the scrubber system via the thickeners.
Overflow from the thickeners is pumped back to the make-up
line for return to the scrubber system.  The sludge curing
ponds provide interim storage while stabilization is taking
place.   One pond receives thickener underflow while a second
is curing and the third is being excavated for final off-
site disposal.
                              3-6

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     A service (river) water system independent from the



power station service water system is provided.  It includes



a pair of 900 gpm, 100 horsepower pumps taking suction from



the existing condenser discharge tunnel and a 10-inch distri-



bution header for the scrubber facility.  It provides fan



spray water, pump seal water, demister spray water, instrumenta-



tion flush water, reagent mixing tank water, and emergency



water for the scrubbers.



     With present loads on the FGD system an excess of water



is entering the system so that closed-loop operation is not



possible.  Excess water is discharged to the bottom ash



settling ponds and from these into the river.  An early



attempt to operate in closed-loop mode resulted in a buildup



in chloride concentration to 4000 ppm, causing significant



corrosion damage to Carpenter 20 steel fan parts, scrubber



internals, and dampers.  Operating parameters are summarized



in Tables 3.1 and 3.2.



3.2  INSTALLATION SCHEDULE



     In December 1969 Gibbs and Hill, Inc. was retained to



conduct a comprehensive study of the most feasible means of



complying with current and anticipated emission regulations



applicable to the Phillips and Elrama Power Stations of



Duquesne Light Company.  In September 1970 Gibbs and Hill



submitted the results of that study indicating that stack



gas desulfurization was the most practical means of achieving



compliance at both stations.  The consultant also concluded



that a dual-stage venturi scrubbing system should be pilot
                              3-7

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             Table 3.1  SUMMARY OF SCRUBBER DATA

                   PHILLIPS POWER STATION
                                        Particulate
                                         Scrubber
                                         Modules
                                  FGD
                                Scrubber
                                Modules
Superficial gas velocity, ft/sec

Module size

Equipment internals

Material of Construction

     Shell


     Internals
                    40

              40'diam x 50'h

                 Venturi
                 Mild steel,
                 Ceilcoted

                 Some 316L
                 stainless,
                 Ceilcoted
              40

           45'diam x 50'h

            Venturi
            Mild steel,
            Ceilcoted

            Some 316L
            stainless,
            Ceilcoted
               Table 3.2  SUMMARY OF TANK DATA

                   PHILLIPS POWER STATION
  Item
No. of units

Unit size

Retention time
at full load

Temperature °F

PH

Solids Cone. %
Materials of
Construction
    Scrubber
  Recirculating
      Tank
20'diam x 30'h

   1.2 minutes


    120°F

       5
  mild steel
   Thickener
70'  diam x 40'
    ambient

      4-6

     40-45
  (Underflow)

  mild steel,
   Celicoted
                              3-8

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tested.  Pilot scrubber specifications were prepared and



issued to five vendors in September 1970.  The successful



vendor, Chemico, Inc., installed a 1500 cfm pilot unit in



February 1971 and completed tests in May of that year.  In



July 1971 Chemico was awarded a contract to build a full



scale system consisting of four particulate scrubbers and a



second-stage SO- absorber connected to one of the four



scrubbers along with lime injection, recycle pump and reheater



equipment.  Gibbs and Hill, Inc. the Architect/Engineer firm



for the project was responsible for the remaining design of



the system.  This construction was completed in July 1973 to



a point where start-up was possible.  The single SO_ absorber



is to serve as a basis for decisions concerning the installation



of additional S02 facilities at the Phillips and Elrama



Stations.  Five particulate scrubbers have been installed at



the Elrama Station.



3.3  COST DATA



     As of April 1, 1975, the system at Phillips represents



a capital investment of approximately $33 million.  It is



expected that an additional $7 million may be required for



additional equipment necessary to comply with the S02



emission limitations.  This cost includes all process



equipment, engineering costs, contractors' fees, and interest



on capital during construction.  This will represent a total



investment of $40 million or approximately $103 per net



kilowatt, exclusive of the costs of additional sludge disposal



facilities that may be required.
                              3-9

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     A recent estimate indicates that the annual operating



and maintenance expenses at Phillips, excluding additional



sludge disposal requirements,  but including fixed charges



estimated at 14.5 percent of capital costs, with full SOj



scrubbing will be about $15 million per year,  or 5.9 mills



per kilowatt hour.



     In an effort to estimate the total capital and operating



costs that would utimately be incurred for the scrubber



system at the Phillips Station, including provision of



adequate sludge disposal facilities for full SO- removal, a



preliminary evaluation was made of the additional property



required for development into a disposal area and the



additional expenses involved in disposing of the sludge.



This estimate indicates total capital expenditures approxi-



mately $147 per KW.



     Present estimates of sludge disposal costs are $5



to $7 per wet ton of sludge (40 percent solids).
                            3-10

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            4.0  FGD SYSTEM PERFORMANCE ANALYSIS






4.1  START-UP PROBLEMS AND SOLUTIONS



     The initial schedule for this installation called' for



start-up of the FGD system on January 1, 1973, to be fol7



lowed by a two-month shakedown period and a ten-month test



period to evaluate the feasibility of the system, so that by



January 1974 decisions could be made regarding additional



equipment installations at the Phillips and Elrama Power



Station.



     Actual start-up lagged the target date by about six



months, and the ten-month test program initiation was de-



layed nearly two years.  A detailed description of the



causes for these delays has been published and is included



in this report as Appendix C.  Problems and solutions are



outlined briefly in the following paragraphs.



     The six month start-up delay was attributed to several



factors.  Some engineering delays occurred as a result of



efforts to incorporate ongoing experience gained at other



Chemico FGD installations.  Equipment delivery delays and



fabrication errors also occurred.  Some defective equipment,



such as fans, had to be field repaired.  Failures of elec-



trical switchgear and transformers occurred during field



tests preliminary to start-up.
                              4-1

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     The scrubber system was put in operation on July 9,



1973, although the lime additive system was not ready at



that time.  Operation without lime resulted in excessive



scrubber liquid acidity that quickly corroded some com-



ponents of the FGD system, including pumps and piping.  The



system operated for two weeks before it was shut down for a



two-week repair period due to a leak in the stack seal.  On



August 5, 1973, the system was restarted with the lime feed



system operational, and ran until October 8, 1973 when it



was shut down until March 17, 1974.



     Scale deposits developed in the scrubbers, and the



scale had to be removed periodically.  Corroded fan dampers



and scrubber cones were Ceilcoted.  Exhaust gas expansion



joints were replaced, fan welds were reground, and stack



mortar joints were repaired.  Many parts were found to be



constructed of off-spec 304 stainless and had to be replaced



with originally specified 316L material.



     An early attempt to operate the system in a closed-loop



mode resulted in a buildup of chloride ion concentration in



the scrubber recirculating system to about 4000 ppm, in-



tensifying the existing corrosion problems and causing



additional ones.



     Installation of the ductwork to the FGD system caused



a flow disruption through the existing ESP so that the



particulate efficiency of the unit was reduced considerably.



This resulted in excessive fly ash carryover into the scrubber



and the consequent generation of excessive quantities of




                              4-2

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sludge.  Additional sludge was also created by treating the



single stage scrubber trains with lime.   As a result the



spare thickener capacity had to be utilized constantly, and



the sludge holding pond capacity was reduced to about a 10-



day fill period as compared to a 28 day design period.  This



situation plus the high outage rate for the stabilizing



agent injection equipment often made it necessary to transport



sludge by truck to the disposal area in a fluid state.



4.2  PERFORMANCE TEST RUN



     A ten-month test program was initiated in December,



1974.  At that time five of the six boilers at the Phillips



Plant were connected to the scrubber system.  This program



will evaluate the efficiency, reliability, and practica-



bility of the system.  A decision should then be made late



in 1975, concerning the installation of additional SO-



removal equipment for compliance with the SO- emission



limitations.  The number of additional second stage ab-



sorbers required for compliance with the regulations will be



determined during the ten-month test program, and this will



establish the completion date for installation of all addi-



tional FGD equipment.



     In the hope of obtaining higher efficiencies of SO-



removal with the use of lime, Duquesne Light is conducting



tests using a lime containing 4 to 6 percent magnesium



oxide.  Various tests on pilot systems indicate that the



higher reactivity of such a lime results in SO2 single-stage



removal efficiencies above 80 percent.  In preparation for





                            4-3

-------
these tests, one of the single-stage scrubbers was isolated



along with one of the thickener tanks.  This isolation was



necessary to establish and maintain the necessary conditions



in the test scrubber and one thickener.  A test run with the



high MgO was made in September, 1974.  However, it has been



difficult to achieve a sufficiently high rate of utilization



of the magnesium oxide.  A few cursory tests under these



conditions indicate SO2 removal efficiencies somewhat better



than those with high calcium lime, but also significantly



less than anticipated.  The tests were suspended in Septem-



ber to further evaluate means of increasing the reactivity



and utilization of the magnesium lime.  Additional tests



with lime in early November showed that better pH control



could be obtained if the lime slurry was heated.  It is



believed that this reagent holds promise, but the tests were



not conclusive because of inconsistencies in the quality of



the lime supplies and the difficulty in blending and obtain-



ing sufficient supplies.



4.3  PERFORMANCE PARAMETERS



     The ultimate S0_ removal efficiency needed to comply



with emission regulations is about 83 percent.  However, the



present equipment installed using only one two-stage system



and three single-stage scrubber trains with lime is pro-



ducing an estimated SO_ removal efficiency of 50-60 percent.



Availability, was reported to be 100 percent in January



1975, but this figure is misleading since there is con-



siderable scrubber redundancy in the system at the present
                              4-4

-------
time.  (Percent availability is defined as 100 times the



ratio of system operating hours to boiler operating hours).



4.4  PROCESS MODIFICATIONS FOR FUTURE INSTALLATIONS



     The design of additional installations will rely



heavily on operating experience gained from this system.



The discussion in Section 4.1 points out many areas where



system improvements can be made, especially regarding



material selection, quality control, and equipment sizing.



Ongoing operational experience during the ten-month test



program will help to optimize process design parameters for



future control systems, if such systems are indicated.
                              4-5

-------
   APPENDIX A




PLANT SURVEY FORM
        A-l

-------
                    PLANT SURVEY FORM

              NON-REGENERABLE FGD PROCESSES


A.  COMPANY AND PLANT INFORMATION

    1.  COMPANY NAME           Duquesno Light Co.	
    2.  MAIN OFFICE            4^5  fiixt-h Avpniie,  Pittsburgh,  Pa.

    3.  PLANT MANAGER          T.S.  Ahhoht	
    4.   PLANT NAME             Phillips Power Station	

    5.   PLANT LOCATION         Cresant Township.  Allegheny County. Pa.

    6.   PERSON TO CONTACT FOR FURTHER  INFORMATION   S.L. Pernick. Jr.
    7.   POSITION                             Manager Environ. Affairs

    8.   TELEPHONE NUMBER                     (412)  471-4300	

    9.   DATE INFORMATION GATHERED           	

   10.   PARTICIPANTS IN MEETING                 AFFILIATION

          Wade  H.  Ponder	              EPA	
          John Busik	              EPA
          Tim W.  Devitt	              PEDCo
          Fouad K.  Zada                      PEDCo
          Robert D.  O'Hara                   D. L. Co,
          I.  S.  Abbott	              D. L. Co.
          R.  G.  Knight	              D. L. Co.
                             A-2
                                                  5/17/74

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B.  PLANT DATA.  (APPLIES TO ALL BOILERS AT THE PLANT).
C.
CAPACITY, MW (Gross)
SERVICE (BASE, PEAK)
FGD SYSTEM USED
BOILER NO.
1 2
35 35
P-B P-B
Wet Gc
3
65
P-B
is Ventui
4
65
P-B
i Scrubb
5
65
P-B
2r
6
148
P-b

BOILER DATA.  COMPLETE SECTIONS (C) THROUGH  (R) FOR EACH
              BOILER HAVING AN FGD SYSTEM.
     1.  BOILER IDENTIFICATION NO.

     2.  MAXIMUM CONTINUOUS HEAT INPUT
                                          1-6
                                         4463
MM BTU/HR
     3.  MAXIMUM CONTINUOUS GENERATING CAPACITY    387     MW  (net)

     4.  MAXIMUM CONTINUOUS FLUE GAS RATE.     2.300.000  ACFM @ 380 °F

     5.  BOILER MANUFACTURER             Foster-Wheeler	

     6.  YEAR BOILER PLACED IN SERVICE    1942-1956	
     7.  BOILER SERVICE  (BASE LOAD, PEAK, ETC.) 	

     8.  STACK HEIGHT                           340' Scrubber Stack

     9.  BOILER OPERATION HOURS/YEAR  (197 )     	

    10.  STATION CAPACITY FACTOR*               70%	

    11.  RATIO OF FLY ASH/BOTTOM ASH            85	
      * DEFINED AS:  Kw" GENERATED TN YEAR
                     MAX. CONT. GENERATED CAPACITY IN KW x 8760 HR/YR
                              A-3
                                                  5/17/74

-------
D.  FUEL DATA

    1.  COAL ANALYSIS (as received)

             GHV (BTU/LB.)

             S %

             ASH %
MAX.
12600
2.8
23
MIN.
10700
1.0
9.5
AVG.
11350
2.15
18.2
    2.  FUEL OIL ANALYSIS (exclude start-up fuel)

             GRADE                      	

             S %                        .	

             ASH %
         N/A
E.  ATMOSPHERIC EMISSIONS

    1.  APPLICABLE EMISSION REGULATIONS

        a)  CURRENT REQUIREMENTS

            AQCR PRIORITY CLASSIFICATION

            REGULATION & SECTION NO.

            MAX. ALLOWABLE EMISSIONS
            LBS/MM BTU

        b)  FUTURE REQUIREMENTS,
            COMPLIANCE DATE

            REGULATION & SECTION NO.

            MAXIMUM ALLOWABLE EMISSIONS
            LBS/MM BTU
PARTI CULA'iES
0.081b/10 BTU
 Same as abov
    SO-
0.6 lb/106BTU
 Article 18 Allegheny County
 County  Health Department
 Same as above
 Same as above
 Same as abovs
        PLANT PROGRAM FOR PARTICULATES COMPLIANCE
          Connect all six boilers to common header to four particulate

          scrubbers
    3.  PLANT PROGRAM FOR S02 COMPLIANCE  Operate 10 months for SO2
        prototype module including single stage scrubbers with lime.
        Based on outcome of tests determine how many additional
        second stage scrubbers required to come into compliance.
        Roughly assume 28 months for second scrubber, 19 months for
        third scrubber, 18 months for fourth scrubber.
                              A~4                   5/17/74

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F.  PARTICIPATE REMOVAL


    1.  TYPE


        MANUFACTURER


        EFFICIENCY: DESIGN/ACTUAL


        MAX. EMISSION RATE*  LB/IIR


                            GR/SCF


                          LB/MMBTU
MECH.
p-r




E.S.P.
R-C




FGD
Chemico
99/N.A.


0.08
        DESIGN BASIS, SULFUR CONTENT
                                               2.3%
G.  DESULFURIZATION SYSTEM DATA


    1.  PROCESS NAME


    2.  LICENSOR/DESIGNER NAME:


                       ADDRESS:


             PERSON TO CONTACT:


                 TELEPHONE NO.:
Lime scrubbing
Chemico Co.
1 Penn Plaza  NY, NY  10001

Paul Chopra	
 (212) 239-5100
    3.  ARCHITECTURAL/ENGINEERS, NAME: Gibbs and Hill, Inc.	


                       ADDRESS:    393 Seventh Avenue NY, NY   10001


             PERSON TO CONTACT:


                 TELEPHONE NO.:
Mr.  Joseph V. Armao
        PROJECT CONSTRUCTION SCHEDULE:
                  DATE
        a)  DATE OF PREPARATION OF BIDS  SPECS.  Pilot scrubber, 9/70


        b)  DATE OF REQUEST FOR BIDS


        c)  DATE OF CONTRACT AWARD               12/70  G&H  7/71 Chemico


        d)  DATE ON SITE CONSTRUCTION  BEGAN       7/71	Phase I
             10/70 pilot,  3/71  full
                              scale
        c)  DATE ON SITE CONSTRUCTION COMPLETED   7/73	


        f)  DATE OF INITIAL STARTUP               July  1973


        g)  DATE OF COMPLETION OF  SHAKEDOWN


     *At Max. Continuous Capacity


                              A-5
               In Progress
               5/37/74
                         Phase I

-------
    6

    7

    8
    LIST MAJOR DELAYS IN CONSTRUCTION SCHEDULE AND CAUSES:

      Equipment delivery, Electrical, Duct Work, Fans	

      I.D.  Fan defects in welds	

      Lack of space to install equipment restricted workers

      Boiler house ductwork erection, method of handling at

        site difficult	

      Selection and development of sludge disposal techniques,

    NUMBER OF S02 SCRUBBER TRAINS USED             1	
    DESIGN THROUGHPUT PER TRAIN, ACFM @ 340 °F   547,000	

    DRAWINGS:  1)   PROCESS FLOW DIAGRAM AND MATERIAL BALANCE
                     See  G  &  Hill  or  Chemico
               2)   EQUIPMENT LAYOUT
H.
S02 SCRUBBING AGENT
    1

    2

    3
    4
    TYPE

    SOURCES OF SUPPLY
                                     Lime
                                     See Dravo Corp.  Mr.  Win.
                                     Lord Neville Island  Pitts,
                                                          Pa.
CHEMICAL COMPOSITION (for each source)
    SILICATES

    SILICA

    CALCIUM OXIDE

    MAGNESIUM OXIDE

    EXCESS SCRUBBING AGENT USED ABOVE
    STOICHIOMETRIC REQUIREMENTS
    5.  MAKE-UP WATER POINT OF ADDITION

    6.  MAKE-UP ALKALI POINT OF ADDITION
                                                      30%
                                         Scrubber Recycle	

                                         Scrubber Vessel Basins
                             A-6
                                                 5/17/74

-------
J .   SC RBERT RAI N SPEC 1FICATIONS
    1.  SCRUBBER NO. 1

        TYPE   (TOWER/VENTURI)           Veniuir i_. .

        L1QUJD/GAS RATIO, G/MCF  @ 120 °F ____

        GAS VELOCITY THROUGH SCRUBBER,  FT/SEC '
        MATERIAL OF CONSTRUCTION                  Carbon Steel	

        TYPE OF L1NJNG                            Ceilcote	

        INTERNALS:

           TYPE (FLOATING BED, MARBLE  BED,  ETC.) Variable Throat  Vonturi

           NUMUKR OF STAGES                     	1	


           TYPK AND SIZE OF PACKING  MATERIAL   	

           PACKING THICKNESS PKR  STAGE*b)


           MATERIAL OF CONSTRUCTION, PACKING:   	


                                     SU P PORTS:	

    2.  SCRUBBER NO. 2 ^

        TYl'K (TOWER/VENTURI)                     Same as 1  	


        LIQUID/GAS RATIO. G/MCF @     °F         	


        GAS VELOCITY THROUGH SCRUBBER, FT/SEC   	 	

        MATERIAL OF CONSTRUCTION                	


           TYPE OF LINING                       	

        INTERNALS:

           TYPE (FLOATING BED, MARBLE  BED,  ETC.)	

           NUMBER OF STAGES                     	


           TYI'i: AND SIXK OF PACKING  MATERIAL    	


 a)  Scrubber No. 1 is the scrubber that  the flue  qascs  first
    enter.  Scrubber 2 (if applicable)  follows  Scrubber No. 1.

 b)  For floating bed, packing thickness  at  rest.


                            A-7
                                                  VI-7/7/1

-------
       PACKING THICKNESS PER STAGE   ^    	  	

       MATERIAL OF CONSTRUCTION, PACKING:	

                                SUPPORTS:__.  	

3.   CLEAR WATER TRAY  (AT TOP OF SCRUBBER)

    TYPE                                 	N_/A_

    L/C RATIO                            _   	

    SOURCE OF WATER                       	
    UEMJSTER

       TYPE   (CHEVRON, ETC.)             	Chevron

       NUMBER OF PASSES  (STAGES)         	

       SPACE BETWEEN VANES               	

       ANGLE OF VANES                    	

       TOTAL DEPTH OF DEMISTER           	

       DIAMETER OF DEMISTER
       DISTANCE BETWEEN TOP OF  PACKING
       AND BOTTOM OF DEMISTER

       POSITION (HORIZONTAL, VERTICAL)

       MATERLAL OF CONSTRUCTION
       METHOD OF CLEANING                	Internal Auto Sprays

       SOURCE OF WATER AND  PRESSURE      	

       FLOW RATE DURING CLEANINGS, GPM  	

       FREQUENCY AND DURATION  OF  CLEANING 	 	

       REMARKS              	            	
5.  REHIIATER

       TYPE  (DIRECT, INDJKECT)         Direct OJ1 Fired

b) For floating bed, packing  thickness at rest.


                        A-8                   5/17/74

-------
       DUTY, MMBTU/HR

       HEAT TRANSFER SURFACE AREA SQ.FT
       TEMPERATURE OF GAS:  IN 	   OUT
       HEATING MEDIUM SOURCE            	No. 2 Oil

            TEMPERATURE & PRESSURE      	
            FLOW RATE                   7.3qal/min LB/ilR

       REIIEATER TUBES, TYPE AND
       MATERIAL OF CONSTRUCTION         	
       REHEATER LOCATION WITH RESPECT  TO DEMISTER  Downstream

        of Demister prior to scrubber  stack  entrance	

       METHOD OF CLEANING 	
       FREQUENCY AND DURATION OF CLEANING
       FLOW RATE OF CLEANING MEDIUM	LB/HR

       REMARKS  Problems with oil pumps,  burners and  temperature

        control so far very  little  operation



6.  SCRUBBER TRAIN PRESSURE DROP DATA        INCHES OF WATER

       PARTICULATE SCRUBBER                  	

       S02 SCRUBBER                          	
       CLEAR WATER TRAY
       DEMISTER                               2"

       REHEATER                              	

       DUCTWORK
       TOTAL FGD SYSTEM
                                              5/17/74

-------
    7.
FRESH WATER MAKE UP FLOW RATES AND POINTS OF ADDITION

   TO:  DEMISTER       Service Water fClarifier)
                QUENCH CHAMBER  Service Water (Clarifier)
                ALKALI SLURRYING   Service Water  (Clarifier)

                PUMP SEALS 	Service Water  (Clarifier)

                OTHER 	
                          Service Water  (Clarifier)
                TOTAL  Make-up service water to thickener overflow
                         tank from river.
           FRESH WATER ADDED PER MOLE OF SULFUR REMOVED    180

    8.  BYPASS SYSTEM                                filank Qff  ^

        CAN FLUIC GAS BE BYPASSED AROUND FGD SYSTEMS But not automatic

        GAS LEAKAGE THROUGH BYPASS VALVE, ACFM  No bypass valve
K.  SLURRY DATA
    LIME/LIMESTONE SLURRY MAKEUP TANK

    I'ARTICULATE SCRUBBER EFFLUENT
    HOLD TANK (a)

    S02 SCRUBBER EFFLUENT HOLD
    TANK (a)
PH



%
Solids



Capacity
(gal)



Hold up
time



L.  LIMESTONE MILLING AND CALCINING FACILITIES:  INDICATE BOILERS
    SERVED BY THIS SYSTEM.

        TYPE OF MILL (WET CYCLONE, ETC.)  Dravo ,Gibbs & Hill	

        NUMBER OF MILLS                  	

        CAPACITY PER MILL                	

        RAW MATERIAL MESH SIZE           	

        PRODUCT MESH SIZE                	
                                                         T/HR
                            A-10
                                                  5/17/74

-------
        SLURRY CONCENTRATION IN MILL          	


        CALCINING AND/OR SLAKING FACILITIES   	


        SOURCE OF WATER FOR SLURRY MAKE UP OR
        SLAKING TANK                          	


M.   DISPOSAL OF SPENT LIQUOR


    1.  SCHEMATICS OF SLUDGE & FLY ASH DISPOSAL METHOD


        (IDENTIFY QUANTITIES OR SCHEMATIC)  	


    2.  CLAUIFIEHS  (THICKENERS)


           NUMBER                           __2	
           DIMENSIONS                         75' diameter


           CONCENTRATION OF SOLIDS IN UNDERFLOW   30-40%


        ROTARY VACUUM FILTER


           NUMBER OF FILTERS                	


           CLOTH AREA/FILTER                	
           CAPACITY                 	TON/111?  'WET CAKE)


           CONCENTRATION OF SOLIDS IN CAKE  	


           PRECOAT  (TYPE, QUANTITY, THICKNESS)  	


           REMARKS	  	 	
    4.  SLUDGE FIXATION
                                            Mixing tank prior to
           POINT OF ADDITIVES INJECTION     sludge holding pond


           FIXATION MATERIAL COMPOSITION    	
           FIXATION PROCESS  (NAME)          Calcilox  (Dravo)	
           FJXATLON MATERIAL REQUIREMENT/TONS OF DRY  SOLIDS  OF  SLUDGE


                                             Nominal 10%  	
                             A-ll                 5/17/74

-------
            ESTIMATED  POND  LIFE,  YRS.
            CONCENTRATION  OF  SOLIDS  IN  FIXED  SLUDGE
            METHOD OF  DISPOSAL OF  FIXED  SLUDGE Truck haul to land fill


            INITIAL  SOLIDIFICATION TIME  OF  FIXED  SLUDGE  	

         SLUDGE QUANTITY  DATA


            POND/LANDFILL SIZE REQUIREMENTS,  ACRE-FT/YR  	


            IS POND/LANDFILL ON  OR OFFSITE    Off-site	

            TYPE OF  LINER                 Hypalon on demonstration
                                                    pond  only

            IF OFFSITE, DISTANCE AND COST OF  TRANSPORT     N/A	

            POND/LANDFILL DIMENSIONS AREA IN  ACRES  	N/A	
                                     DEPTH  IN FEET  	N/A	


            DISPOSAL PLANS; SHORT  AND  LONG  TERM     	
N.   COST DATA
                                        $33,000,000 Phase I,
     1.   TOTAL INSTALLED CAPITAL COST  Phase II -$7.000.000 	
                                        without fixed charges Phase I is
     2.   ANNUALIZED OPERATING COST     S5fQQQfQQQ Phase II 7.273.000
                                        Including fixed charges Phase I
                                        10,000,000 Phase II 13,661,000
                             A-12                  5/17/74

-------
3.
COST BREAKDOWN
      A.
COST ELEMENTS
CAPITAL COSTS
S02 SCRUBBER TRAINS
LIMESTONE MILLING
FACILITIES
SLUDGE TREATMENT &
DISPOSAL POND
SITE IMPROVEMENTS
LAND, ROADS, TRACKS,
SUBSTATION
ENGINEERING COSTS
CONTRACTORS FEE
INTEREST ON CAPITAL
DURING CONSTRUCTION
ANNUALIZED OPERATING COST
FIXED COSTS
INTEREST ON CAPITAL
DEPRECIATION
INSURANCE & TAXES
LABOR COST
INCLUDING OVERHEAD
0 & M COSTS
LABOR
RAW MATERIAL
UTILITIES
MAINTENANCE
INCLUDED IN
ABOVE COST
ESTIMATE
YES
a
X
a
X
a
x
a
X
a
X
E
NO
a
a
a
a
a
a
n
a
a
a
s
a
a
a
ESTIMATED AMOUNT
OR 1 OF TOTAL
INSTALLED CAPITAL
COST
G & H











7.5%
20.5%
19.0%
	 15.5% 	
            DISPOSAL
                                                  37.5%
     Based on full S02 removal to meet regulations of
     0.6% Ib S0-/million BTU emissions.
                             A-13
                                                      5/17/74

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     4.   COGT [-'ACTORS

          a.   ELECTRICITY

          b.   WAT UK

          C.   STEAM (OR FUEL FOR  REHEATING)

          d.   FIXATION COST    N/A	
                                         X
          C.   RAW MATERIAL PURCHASING  COST

          f.   LABOR:  SUPERVISOR        	

                      OPERATOR          	

                      OPERATOR HELPER   	

                      MAINTENANCE       	
                                    S/TON OF  DRY SLUDGE

                                    	 $/TON  OF DRY SLUDGE

                                    _ HOURS/WEEK	WAGE
U.   MAJOR PROBLEM AREAS:   (CORROSION,  PLUGGING,  ETC.)

     1.   S02  SCRUBBER, CIRCULATION TANK  AND PUMPS.

          a.    PROBLEM/SOLUTION	
                .Deposits on  skirts  of  scrubber, Gusset Plate
                Throat parnper_ __	
                Under Upper  Cone	
     2.
      3.
     Bleed Valves	
     Recycle  Pumps_
DEMISTER
     PROBLEM/SOLUTION,
     Lime Deposits
REIIEATER
PROBLI-:M/SOLUTION_	_ .
     J?.unip_s_, __Blo.wer.s.,_..Tenip_. .Co_ntr_ol
                               A-14
                                                    5/17/74

-------
4.    VENTURI SCRUBBER, CIRCULATION TANKS AND PUMPS

     PROBLEM/SOLUTION	
     Recycle pumps_  33% Impeller and  casing  erosion in 3000 hrs
       Better volute design, possibly rubber line pumps	
5.   I.D. BOOSTER FAN AND DUCT WORK

     PROBLEM/SOLUTION	
      Dampers  Corrosion  - Ceilcote  same
      Fan  Yiflrf  s-t-rp»nnhh .  r^nrrnsinn  —  rnhhpr 1 i np shaft:,  Tnf-prp
         _           ^  f—                             '    Wash
      Exp. Joint  .Asbestos-Butyl  compound material for joints	
        better than  s.s.
      Fan Strengh^LWeld mat overlay  install  doubler plates to
        reduce operating yield  strength	

6.   LIMESTONE MILLING SYSTEM OR LIME  SLAKING
     PROBLEM/SOLUTION	
     Degritting  -  No  redundancy  10%  down time	
     	better  if indoor  operation,  spare capacity	
7.   SLUDGE TREATMENT AND DISPOSAL

     PROBLEM/SOLUTION	
           .Over_ 10OQ_ton/day sludge disposal requir_ed_t Purchase
       and  Development	
      Leachate  Still not known if leachate is acceptable	
       more testing  required.	 		
                       A-15                   5/17/74

-------
     8.   MISCELLANEOUS AREA  INCLUDING BYPASS SYSTEM

          PROBLEM/SOLUTION	
           Instrumental:!On  need good pH cells, constant  attention
             .  stack opacity monitor useless
           Boiler Instrument	
           Stack
           Noise  Fan noise and associated equipment
           InstrumentativG    Sump pumps high erosion wear
     DESCRIBE FACTORS WHICH  MAY  NOT  MAKE THIS A REPRESENTATIVE
     INS TALL AT I ON    What is representative?  No  such thing
      Possibly Land limitations	
Q.   DESCRIBE METHODS OF  SCRUBBER CONTROL UNDER FLUCTUATING
     LOAD.  IDENTIFY PROBLEMS  WITH THIS METHOD AND SOLUTIONS.
     IDENTIFY METHOD OF pH  CONTROL AND LOCATION OF pH PROBES.

     Boiler gas _flow._ fed into damper  control  and  venturi  throat ___

     damper control.   System has worked ok. but because plant  hag only

     jr.ecejitJ.Y-r.un.. with all, boilers rnnnect'p'ri  t-O g
      had in_s.ufficie_nt_time_ to. observe. _ Have lost  trains  occasionally
      pH  is controlled by maintaining scrubber .re_cy_cle .solution., at a
      given level.           _                _ _   _      _
                              A-16                 5/17/74

-------
   APPENDIX B




PLANT PHOTOGRAPHS
        B-l

-------
Photo No. 1  General view of the Phillips Power Station from
the sludge disposal area.  The scrubber stack appears at the
center of the picture.
 Photo No.  2  View of the Phillips lime storage tank and
 slaking facility.  The storage tank has a   -day capacity
 of       pounds of lime.
                         B-2

-------
   Photo  No.  3   View  of  the  Phillips  FGD  scrubber module  is
   almost completely  obscured  by  structural  steel.   Gas inlet
   duct appears  at  the right side slightly below the center  of
   the picture.
Photo No. 4  View of ductwork between scurbber and stack.
The direct-fired reheater is located immediately to the right
of the scrubber module.

                              B-3

-------

 Photo No.  5  View of Phillips  FGD scrubber recirculating  pumps
                                       ?t ***
                         Pf ft  '  Jt* *Ji-*'*;
Photo No.  6  View of the Phillips scrubber  control panel
                          B-4

-------

Photo No. 7  View of edge of empty Phillips sludge disposal
pond showing plastic barrier liner which surrounds the pond.
Leachate collection pipes are installed in the bottom of the
pond for sampling and analysis.
 Photo No. 8  Stabilized sludge in Phillips test disposal
 pond.  Barrier liner at perimeter can be seen in foreground
 and background.
                          B-5

-------
    APPENDIX C




OPERATIONAL REPORT
        C-l

-------
   DUQUESNE LIGHT COMPANY
   PHILLIPS POWER STATION
   LIME SCRUBBING FACILITY
              By
        Steve L.  Pernick, Jr
    Manager-Environmental Affairs
        Duquesne  Light Company
       Pittsburgh, Pennsylvania
              and
        R.  Gordon Knight
 Superintendent-Technical  Services
      Duquesne Light Company
     Pittsburgh, Pennsylvania
     Prepared for presentation
              at
EPA Flue Gas Oesulfurization Symposium
        Atlanta, Georgia
       November 4-7, 1974
              c-2

-------
                       DUQUESNE LIGHT COMPANY
                       Phillips Power Station
                       Lime Scrubbing Facility
                             CONTENTS

                                                            Page
Introducti on	V-4
Pilot Plant Operation  	C-5
Installation Schedule	C-6
Description of System  	.C-8
Initial  Operation 	C-ll
Extended Shutdown for  Repairs	C-13
Second Start-up Operation	C-16
Sludge Treatment and Disposal	C-18
Future Operating Plans	C-21
Availability and Reliability	C-23
Capital  and Operating  Expenses	C-23
Future Objectives	C-24
                              c-3

-------
                           DUQUESNE LIGHT COMPANY
                           Phillips Power Station
                           Lime Scrubbing Facility
INTRODUCTION

          Duquesne Light Company is an investor-owned electric utility
serving approximately 1/2 million customers in southwestern Pennsyl-
vania including Pittsburgh.  The Company has a net generating capa-
bility of approximately 2700 MW and presently operates three coal
burning power stations, two of which, Phillips and Elrama,  are dis-
cussed in this paper.

          In 1969, Gibbs & Hill, Inc.  was engaged to conduct a com-
prehensive study of the most feasible means of complying with:  the
emission regulations being promulgated at the time by Allegheny County,
which has control over the Phillips Station; the regulations of the
Commonwealth of Pennsylvania, which has jurisdiction over the Elrama
Station, and the most stringent regulations that could reasonably be
conceived.  The study was completed in September, 1970.   It repre-
sented a comprehensive evaluation of all test data concerning emis-
sions from the two power stations and an intensive investigation of
all possible means of compliance with the applicable and anticipated
regulations.  The study concluded that:  (1) the use of low sulfur
western coal was not a feasible means of compliance since it would
not achieve compliance with the particulate emission limitations of
the regulations with the existing dust collection equipment; (2) that
conversion from coal to low sulfur oil was not feasible due to the
uncertainties of obtaining a sufficient supply of the necessary
large quantities of such oil; and (3) that the most practical means
of sulfur dioxide emission control was desulfurization of stack
gases.  The consultants then conducted a thorough study of existing
methods of sulfur dioxide removal from stack gases.  At the time of
their investigation in 1969 to 1970, only two full scale stack gas
scrubbing systems were in operation in the United States.  One of
these has since been abandoned and the second has had a poor record
of operating reliability.  Furthermore, the injection of limestone
directly into the boiler, which was the basis of these SO? removal
processes, was not at all suitable for consideration at the Elrama
and Phillips Power Stations since it would result in additional
boiler tube erosion to which the boilers were already particularly
susceptible.  Furthermore, available data indicated that S02 removal
efficiency might not be sufficiently high to comply with the regu-
lations which were among the most stringent in the country.

          Because of the characteristics of our boilers and our re-
quirements for a system that would remove both particulars and sul-
fur dioxide, the report concluded that a tail-end scrubbing system
was the best available means of control and recommended that we in-
stall a dual stage venturi scrubbing system.  Some of the technical


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reasons for choosing the system are as follows:

  1.  It was thought that a dual stage scrubbing system would enable
      separating the sludges resulting from scrubbing for fly. ash
      in the first stage and scrubbing for S02 in the second stage,
      in the event the sludge from the S02 removal stage became a
      problem.

  2.  A dual stage scrubber had the potential of being converted
      to a magnesium oxide regenerative system in the event it
      became desirable or practical to do so.

  3.  Venturi scrubbing for particulate removal was fairly well
      proven in the steel industry.  Furthermore, if only one
      of the scrubber trains was equipped with a dual stage S02
      prototype, and this was proved to be impractical or un-
      workable, we would still have a workable single stage ven-
      turi scrubber system for particulate removal.  We could
      then investigate an alternate method of S02 removal with
      minimal loss of investment.

          In addition to the above reasons was the fact that preliminary
time schedules indicated that these scrubbers could be delivered with the
least delay.  Duquesne accepted the recommendations of Gibbs & Hill, and
in view of the unproven nature of the wet scrubbers for sulfur dioxide
removal, decided that the most prudent approach to the installation was
to begin by equipping only a portion of the scrubber system at the Phillips
Station with sulfur dioxide removal equipment.  Subsequently, Gibbs & Hill
was instructed in September, 1970, to proceed with the designing and in-
stallation of the Phillips scrubber system.  The scrubber installation
at this plant was to include four scrubber trains.  Three of these were
single stage scrubbers for dust removal, and one was a dual stage scrub-
ber (two single stages in series) which is the prototype for sulfur di-
oxide removal.  Each scrubber was to be capable of approximately 540,000
CFM, which is the equivalent of approximately 125 megawatts.  With the
station rated at 387 megawatts, this meant that the station would be
equipped with essentially a spare scrubber train.  This was a criterion
specified by Duquesne Light Company to assure sufficiently high avail-
ability of the system.

          It was anticipated that after a trial period, the operation of
the prototype would serve as a basis for decision as to the installation
of additional similar S02 removal equipment at this station and other
coal burning facilities to comply with the applicable regulations.

PILOT PLANT OPERATION

          In February, 1971, a pilot plant size Chemico venturi type,
dual stage scrubber system with a capacity of 1500 CFM was installed
at the Phillips Power Station to study the performance and operating
characteristics of the dual stage venturi scrubber system.  The pilot
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plant was connected to the duct entering the mechanical  dust collector
of No. 5 boiler.  The scrubber was operated with various types of lime-
stone and lime.  In addition, other conditions such as the stoichiometry,
liquid to gas flow ratio and pressure drop were varied in order to deter-
mine the conditions which would yield optimum collection efficiency and
operating conditions.  After determination of these parameters in approxi-
mately 3 months of operation, the pilot scrubber was dismantled on May 8,
1971.

          In the meantime, in March, 1971, invitations to bid were issued
by Duquesne Light Company to Chemico and Combustion Engineering for a
scrubber system capable of removing sufficient S02 and particulates to
comply with existing and anticipated future regulations.   The bid was
subsequently awarded to the Chemico Corporation in July, 1971.  The
battery limits for Chemico was limited to the scrubbers  and associated
pumps and controls between the inlet hot gas duct manifold to the exit
wet gas header, including the reheater but excluding the new induced
draft fans.

          In obtaining approval of our plan, compliance  programs were
negotiated with Allegheny County for the Phillips Station and with the
State for the Elrama Power Station.  The program included the instal-
lation of five single stage venturi scrubbing trains for particulate
removal only at the Elrama Station, to be installed concurrently with
the Phillips scrubber system as described above.  The plan was to use the
prototype sulfur dioxide removal installation at Phillips as a basis for
decisions concerning additional SC>2 removal equipment at both stations
in order to comply with SC>2 emission limitations.

INSTALLATION SCHEDULE

          Although in Diiquesne's best judgment, the scrubber system could
not be made operational, even for particulate removal, prior to July 1,
1973, which was 34 months from the date of our decision  to install a
scrubber system, Duquesne Light eventually acceded to pressure from the
State of Pennsylvania and established a target date of January 1, 1973.
Following startup, the schedule called for a tv/o-month "debugging" period
followed by a ten-month test program on the prototype SO^ scrubber at
Phillips.  This would determine if stack gas scrubbing with alkaline in-
jection on a plant scale basis was a feasible and reliable means of re-
moving sulfur dioxide from the gases.  The plan was to study operating
conditions during this period to establish optimum SC"2 removal efficiency
using various types of lime, the operating mode most conducive to reliable
trouble-free operation, and other essential information.  The schedule
called for a decision to be made by January 1, 1974, as  to whether or not
the operation of the prototype S02 scrubber was satisfactory or if an
alternate system should be investigated.  If the operation of the prototype
sulfur dioxide scrubber proved satisfactory, the schedule called for design,
procurement and installation of additional SO? removal equipment by January 1,
1975, for both stations.  At that time, compliance with  County and State
regulations would be achieved.  (For a list of significant dates see Figure 5)
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          Despite our best efforts, no part of the Phillips scrubber
installation was placed in operation until  July 9, 1973, and then for
only two boilers.  At that time, two of the scrubber trains were
placed in operation, and tv/o of the six boilers were connected to the
scrubber system.  This was consistent with our startup schedule which
called for connecting one boiler at a time to the scrubber system so
as not to jeopardize the availability of a significant portion of the
plant's generating capability in the event of failure of the scrubber
system.  The tv/o boilers connected have a combined steam generating
capability equivalent to approximately 80 megawatts.

          The July 9, 1973 startup date represents a slippage of approxi-
mately 6 months from the original schedule.  This slippage was attribut-
able to the following factors:

  1.  The venturi scrubber system was not a completely engineered
      system at the time it was purchased,  and a considerable amount
      of developmental engineering was required to adapt the scrubbers
      to a system that would meet our requirements.   Chemico was al-
      so charged to incorporate, to the limits of their responsibility the
      latest available operating and maintenance experiences at the Four
      Corners Plant in New Mexico, the Dave Johnston Plant in Wyoming,
      Mitsui Plant in Japan, and any other  Chemico installation having
      experiences adaptable to our proposed installations.

  2.  Equipment suppliers and fabricators did not meet promised de-
      livery dates due to the volume of orders, decreased produc-
      tivity, and inadc  'ate quality control.  Considerable money
      was spent to expccite and inspect equipment and materials for
      our project.  In spite of this effort and expense, many late
      deliveries and mistakes in fabrication occurred.  Some examples
      are as follows:

      a.  The induced draft fans were scheduled for delivery
          in Phillips by July 15, 1972.  Delivery was not
          completed until December 12, 1972, a delay of five
          months.  Not only were the fans late, but numerous
          cracks and defects in the welds on the fan rotors
          were found after delivery.  It was necessary to
          grind out all of the defective welds and make the
          necessary repairs in the field.

      b.  An approximate five-month delay was experienced in
          delivery of the ductwork.  In addition, because of
          the huge size and weight of the ductwork,  many
          structural support schemes had to be studied before
          an acceptable method of reinforcing the existing
          station building to accept the unusual weight load
          of the ductwork could be determined.  After a rein-
          forcement plan was devised, errors were discovered
          in the implementation of the plan, requiring cor-
          rective design work.

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      c.  Delays of up to six months were experienced in the
          delivery of electrical equipment such as switch-
          gear and transformers.  In addition to the delay
          of equipment, errors were found in the wiring dia-
          grams for this equipment.  Once the equipment was
          received, design errors were also discovered, such
          as improperly designed bus connections on the switch-
          gear and improper alignment of bus bars on power
          centers.  In addition, failures of switchgear and
          transformers were experienced during field testing.

      These are only a few examples of the numerous delays and errors
      by equipment suppliers which affected the final completion date
      of the first phase of the Phillips project.

  3.  Major delays were also incurred in the field, such as the follow-
      ing:

      a.  Because of engineering delays and late delivery of
          equipment, construction schedules had to be con-
          tinually revised which seriously affected pro-
          ductivity.

      b.  Space limitations existing at the job site, more
          serious than anticipated, affected productivity
          because of the lack of accessability and maneuver-
          ability.  Special equipment and construction methods
          for the installation of the equipment were required
          beyond those originally anticipated, thus contribu-
          ting to additional delays.

      c.  The availability of boiler outages for tie-in of the
          new ducts, presented additional problems.  Outages
          had to be scheduled months in advance, and any re-
          vision in schedule was dependent upon availability
          of purchased power and the outage schedules of
          other generating equipment, both on our system and
          on interconnections.

DESCRIPTION OF SYSTEM

          Design of both the Phillips and Elrama systems was a joint
effort by Gibbs & Hill and Chemico, each having certain battery limits.
Construction was the responsibility of Gibbs & Hill.  Only the Phillips
system will be described in detail.

          The Phillips system comprises four parallel trains,  Figure 1,
and was designed to handle a total gas volume of 2,190,000 ACFM with
all trains in service.  With one train out of service, the three
trains have a capacity of 1,600,000 ACFM, which is sufficient  for
400 MW, assuming normal excess air.
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          Three scrubber trains were provided with first stage scrub-
bing for fly ash removal, Figure 2.  The fourth train, known as the
"prototype" SOp train, was fitted with a first stage particulate re-
moval scrubber and a second stage SOo absorption scrubber as shown
on Figure 3.

          The ductwork on each boiler was modified to enable operation
with the gases going either to the scrubbers or to the original gas
path after passing through the existing dust collection equipment.
A mechanical and electrical dust collector are located in series
ahead of each individual boiler stack.  The existing ducts leading
to the old ID fans and stacks were blanked off with removable steel
plates to enable diversion of the flue gas to a new common duct.
The new ductwork is routed to the scrubber building where 16 foot
diameter takeoffs lead to each of the four first stage scrubbers.

          The hot flue gas (about 340°F) containing fly ash and sul-
fur dioxide (about 1400 ppm S02) enters the first stage scrubber and
impinges upon the upper cone.  One half of the total scrubber liquor
(8250 gpm) is introduced, Figure 4, into the vessel through the bull
nozzle where it is sprayed over the surface of the upper cone, to
initiate the scrubber action.  A second stream of 8250 gpm scrubber
recycle liquor enters through the tangential nozzles at a point
above the adjustable throat damper.  The flue gas and scrubbing
liquor are brought into intimate contact in the throat section of
the scrubber where ths particulates and some 862 are removed.  The
gas and liquor continue downward to the separator section where, after
being separated from the scrubbing liquor, the flue gas enters a de-
mister where entrained liquor is removed.  The gas leaves the-scrubber
and enters a new wet ID fan which is provided with water sprays to re-
move any accumulation of solids resulting from carryover from the
scrubber.  Fresh water is used for spraying.

          The ID fan housings are lined with 1/4 inch thick natural
rubber.  Wheel material is Carpenter 20 Cb 3.  The shaft is 316 L
stainless steel.  Each fan is driven by a 5500 HP, 1200 RPM, 4160V
electric motor.  Bearings are of the water-cooled type, served from a
closed  cooling water system.

          Outlet gas temperature, normally 110-120°F, from the first
stage scrubber is monitored.  At 175°F a control valve is automatically
opened to admit emergency cooling water to the upper cone.  Additional
temperature rise would automatically shut down the fan and close the
isolation dampers.

          The gas leaving the ID fan enters one of two vessels de-
pending on the train.  In the case of the three single stage scrubber
trains, the gas enters an entrainment separator in which entrained
water is separated and collected.  The separators or mist eliminators
are separate vessels which will be replaced by second stage scrubber
vessels if the test program indicates this to be necessary,  in the
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case of the S02 prototype train, gas leaving the ID fan enters a
second stage scrubber vessel, which is identical in size and design
to the first stage.  This second stage vessel  is equipped with a
reagent (lime) injection nozzle in the bottom cone.  The scrubbing
liquor is then picked up by the two recycle pumps  (Carpenter 20
Cb 3).  Some of the liquor is bled off to the first stage scrubber, where
some is removed from the cycle to thickeners,  and the balance is
recycled.

          Total recycle flow is about 16,500 gpm with a 615 gpm
bleed to the thickeners.  All single stage vessels have also been
fitted with reagent nozzles and feeds to enable control of pH and
incidental S02 removal.

          The exit gases leaving either the second stage scrubber
vessel orthemist eliminator vessel enter a common wet duct lined
with Flakeline 103 (a product of the Ceilcote Company consisting
of a glass flake filled modified polyester resin, subsequently
referred to as Ceilcote) which leads  to a new concrete acid re-
sistant brick lined chimney.  Prior to entering the 340 foot
chimney, a section of the wet gas duct, constructed of 316L SS is
equipped with a reheater, employing a direct oil-fired burner system.
The two-burner system is capable of reheating 30°F, although the in-
tent is to normally reheat 20°F.

          Bleed off from all scrubbers is directed to a trough feeding
two 75 foot diameter thickeners.  The overflow from these thickeners
is directed to a collecting tank where it is pumped by two-2000 gpm
SS pumps to the make-up line for return to the scrubber system.

          Thickener underflow, at 35 to 40% solids concentration, is
pumped by one of two 105 gpm, 15 HP pumps to one of three clay lined
sludge holding ponds.  Each pond has a capacity of about 6500 cubic
yards.  Just prior to discharge to the holding ponds, the sludge
enters a mixing tank where a stabilizing agent can be added at a
predetermined rate based on the density of the sludge as it leaves
the thickener.  After the additive is intimately mixed with the
sludge, the mixture discharges by gravity to one of the ponds.

          In the pond, both settling and curing take place.  Super-
natant liquid is withdrawn and recirculated to the scrubber system
via the thickener.  The sludge curing ponds provide interim storage
while stabilization is taking place.  One pond received thickener
underflow, while a second is curing and the third is being excavated
for final off-site disposal.

          Lime is fed from a storage silo at a controlled rate to the
lime slaker where it is slaked with fresh make-up water.  The slaked
lime overflows into a slaker transfer tank, where make-up water is
added to provide a constant flow of lime slurry with a concentration
of about 15%.
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          A service (river) water system independent from the power
station service water system is provided.   It includes a pair of 900
gpm, 100 HP pumps taking suction  from Lhs existing condenser dis-
charge tunnel and a 10 inch distribution header for the scrubber
facility.  It provides fan spray water, pump seal  water, mist elim-
inator and scrubber demister spray water,  instrumentation flush
water, chemical mixing tank, and emergency water for scrubbers.

INITIAL OPERATION

          Although the lime addition system was not yet completed,
partial start-up of the scrubber system began on July 9, 1973.   The
decision to proceed with startup, without  the lime addition system,.
was made in light of the fact that wo thought the scrubber system
was suitable for operation at a low pH.  Almost all of the major
components and piping were either Ceilcoted, rubber lined or fabri-
cated of a corrosion resistant material to withstand a low pH.
During the first five days of operation, a pH of approximately 1.3
to 2.0 developed in the scrubbing liquor c/hile burning 1.8-2.0% sul-
fur coal.  Because of pressure to prour_>d  with the debugging operation,
and because of our reluctance to incur additional  delays, the decision
was made to continue operation with the low pH rather than shut down
the scrubbers until the lime system became operational.  Unfortunately,
as a result, the scrubber system was forced out of service due to the
corrosion failure after five days of the two thickener overflow re-
turn pumps, which were intended for operation at a pH of 5  to 6.  They were
promptly replaced with two 316 L SS purrps.  Use of the lime system
feed to the thickeners was obtained after  the first week of operation.

          During the first two weeks of operation, additional problems
developed and were corrected in a two-week outage following the first two
weeks of operation:

  1.  A piece of rubber linrr was found in the suction of one of
      the recycle pumps.  The individual scrubber was shut down
      in an effort to locate the source; however, it could not
      be determined until  the corrosive nature of the scrubber
      media  caused the failure of a 20"/16' Tee within 10 days.

  2.  Leaks occurred in the lead floor lining of the stack which
      were a potential threat tu the stack (oncrete structure.
      The lead sheets had been solder-r! rather than "burned."
      The lining was replaced.

  3.  Leaks developed in four 405 *5S expcinsion joints in the
      gas ducts leading to the stack.  The appearance of the
      failed metal was variously escribed cis that of "lace
      curtain" or "swiss cheese."  Fhi., resulted from partial-
      load type of operation of the scrubber system requiring us
      to partially open t^c vacuum breakers and allow ambient air
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      to supplement the gas flow through the scrubbers.   Conden-
      sation resulted.  The joints were replaced with an asbestos/
      butyl material.

  4.  The reheater, which utilizes direct firing of No.  2 oil  in
      the cold gas duct as it enters the stack, is not yet oper-
      ational.  We have been unable to obtain satisfactory oper-
      ation of the reheater due to burner problems and oil pump
      problems.  We have placed no priority on solving these prob-
      lems due to our reluctance to operate the reheater consid-
      ering the present energy crisis and oil shortage.   Whenever
      the reheater becomes operational, we plan to operate it
      during periods of adverse meteorological conditions to ob-
      tain a higher effective stack height.

  5.  During the outage, evidence of corrosion was found on the
      ID fan shaft shrouds, inlet dampers and stiffener bars - all
      316 L stainless steel.  TWO corrective measures were taken -
      redesign of the fan sprays and application of 1/4-inch
      rubber coating to the affected parts.  After two weeks of
      operation the chloride concentration in the liquor (closed
      cycle)had reached 800-900 pprn.  This, no doubt, contributed
      to the corrosion noted above.  It was eventually to reach
      3500-4500 ppm.

          On August 5, 1973, the scrubber system was returned to service
with the lime feed system for pH control continuing in operation.  In
addition to No. 1 and No. 2 boilers, the No. 3 boiler was also connected
to the scrubber system, which made a total of approximately 145 mega-
watts.

          During the following weeks of operation, we were informed by
Chemico of a major change in the operating requirements of the scrubbers;
namely, the necessity to bleed more fluid to the thickener tanks so
that the concentration of solids in the recycling fluid could be kept
to a minimum in order to protect the recycle pumps, and to minimize the
settling of solids in the bleed lines.  This caused a change in the de-
sign concept by essentially doubling the bleed rate.  This meant that
the two 900 gpm thickener tank overflow return pumps, which had been
provided with the system, were inadequate since they no longer had
sufficient capacity to supply the needs of the scrubber system under
one pump operation (the second being a spare) with all boilers con-
nected to the scrubber system.  Two 2000 gpm pumps were obtained for
later installation in parallel with the two 900 gpm pumps.

          During the two months of operation following the August 5,
1973 start-up date, operation of the scrubbers was alternated between
trains.  In other words, as problems arose on one train, it was shut
down and another train was put in service to take its place.  No effort
was made to operate the dual stage prototype S02 scrubber for full SOg
removal because it was felt that debugging operations could more effect-
ively proceed with the most basic operation possible, in other words,

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with the single stage scrubbers.

EXTENDED SHUTDOWN FOR REPAIRS

          During the operation of the scrubbers  in  August  and  Septem-
ber, 1973, additional problems came to light which  caused  an extended
shutdown of the scrubber system,  and a further delay in  the operating
schedule, namely:

  1.  A routine inspection of the new stack revealed additional
      moisture leaks from condensation (pH 2.0)  seeping  through
      the mortar joints and running down  the outside of  the acid
      brick lining.   Seepage was  occurring in more  than  100 areas
      of the brick lining.   The condensate was collecting  at the
      bottom of the  stack in the  annul us  between the lining and
      the shell.  The acid condensate was also seeping through
      construction joints and down the outside of the concrete
      shell permitting it to attack the concrete, which  could
      possibly impair the structural  stability of the stack.   The
      contractor advised us that  a four week outage would  be
      necessary to permit inspection  of all  mortar  joints  and
      to repoint as  required.   This outage for other reasons to
      be described,  extended for  about five months.

  2.  Significant scaling and buildup had occurred  in various
      portions of one or more of  the  scrubbers and  in the  asso-
      ciated piping  in varyimj degrees as described below:

      a.  Buildup was found on many of the upper cone sup-
          port struts.  These football-size accumulations
          appeared to be creating a disturbance  in  the water
          flow pattern over the cone  resulting in accumu-
          lations of deposit en the cone  surface.

      b.  Deposits were found in  the  throat area of two  of
          the scrubbers, sufficiently thick in some areas
          to prevent the maintenance  of the six  inch de-
          sign pressure drop across the throat.

      c.  A thin buildup of hard  scale was observed on the
          face of the throat dampers  of on? of the  scrubbers.

      d.  Deposits of fly ash were found  in and  around the
          operating  mechanisms of the adjustable throat
          dampers.   These were sufficient to prevent full
          adjustment of the dampers.

  3.   Corrosion/erosion was found in  numerous  areas:

      a.  Severe pitting and corrosion  appeared  on  all of  the  316 L
          clad ID fan damper blades and frames.   The cladding  was
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        removed and the carbon steel  was Ceilooted.

    b.  In all scrubbers, a moist layer of fly ash was observed
        on the carbon steel skirt that directs the flue gas
        down the cone.   Extensive rusting was found under the
        fly ash and on  the underside  of the vessel tap as well.
        The latter may  have resulted  from frequent outages for
        inspection, during which alternate wetting and drying
        occurred.

    c.  The upper cones of the scrubber vessels were fabricated
        with a 316 L SS apex.   The balance was carbon steel with
        a Ceilcote coating.  The uncoated apex showed erosion/
        corrosion in all vessels.  Similar attack was shown on
        the inner surface of the 316  L bull nozzle directly
        above the  cones.  Both affected areas were coated during
        the outage.

    d.  Baffle plates in some tangential nozzles (12 per vessel)
        were found badly corroded.  The specified material of
        construction was 316 L SS, but it was found that the
        corroded baffles had been fabricated  of 304 SS.  Six-
        teen baffles out of a total of 60 required replacement
        with 316 L.

    e.  Similarly, the  throat damper  arms (12 per vessel) were
        supposed to be  316 L SS.  Thirty-two  out of a total of
        60 were badly corroded and were found to be 304 SS.  They
        were replaced with 316 L.

    f.  The top and bottom throat damper scraper blades were
        practically destroyed.  The also were found to have
        been 304 SS instead of 316 L.  They were replaced with
        316 L.

4.  An initial inspection and analysis of the ID fans by Franklin In-
    stitute Research Laboratory (FIRL) indicated the existence of
    chloride stress corrosion cracking of the parent metal and
    structural welds, as well  as general corrosion on all exposed
    surfaces.  At that  time, they advised us  that the problems re-
    sulted from the hostile environment in which the fans were
    operating.  In addition, they made a specific recommendation
    that the fans not be operated in  the condition found at that
    time, due to possible catastrophic failure.

      As a result of their search for protective coatings, FIRL
    recommended the application of a  Ceilcote material, Coroline
    505AB.  This is a hard, impervious, acid  resistant, epoxy base
    material which is applied at a nominal thickness of approxi-
    mately 1/4".  The application of  the Coroline is a tedious,
    time consuming hand application by trowel and requires close


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      quality control.  The application of the material  began in
      November, 1973.  Although Coroline had not been extensively
      used on fan blades, or proven to any degree, we were given
      reasonable assurance that it would be successful.   As a
      result, we began application of this material to as many
      fans as manpower permitted.

        On January 22, 1974, the first fan was completely coated
      and was started up for balancing.  After a balance move
      was attempted, the fan was forced out of service due to
      excessive vibration resulting from separation of a portion
      of the coating from one of the blades.  The Ceilcote Com-
      pany informed us that the separation was localized and
      probably caused by a faulty batch of material which did
      not properly adhere to the metal. The Coroline was re-
      applied and the fan was started again on February 5, 1974
      and again was forced to shut down due to separation of the
      material in a second area.  At that time, the Ceilcote Com-
      pany was unable to adequately explain the failure of the
      coating to adhere to the fan surfaces.  As a result, the
      decision was made that the application of Coroline as
      protection against the adverse effects of the flue qases
      was not the answer to the problem. It is believed that the
      flexing of the blades during operation may have contributed to
      the lack of adhesion between the Ceilcote and the blades.

        By this time, FIRL had been able to conduct more exhaustive
      investigations and analyses on the fan blade material.  As a
      result, they revised their initial conclusion and reported
      that the fans were suffering from a much lesser degree of
      stress corrosion cracking of the weld metal and a degree of
      pitting attack on all fan blades.  The report also indicated
      that fen failure was no longer considered imminent.

          In review of the ID fan problems, it appears that the corrosion
problems which we had experienced might be partially due to the operation
of the scrubber system at a lower pH and a higher chloride concentration
(3500-4500 ppm) than had been foreseen by the scrubber designers.  Several
steps were taken to try to alleviate the situation:

  1.  Operation of the dual stage scrubber with full lime addition,
      which we felt would be adequate for maintaining optimum pH
      control in that train;

  2.  Addition of supplemental lime feed to the other operating
      scrubbers, and

  3.  The installation of a redesigned spray system, which had proven
      effective at other installations.
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    These steps in addition to frequent scheduled fan inspections
    were felt to be adequate safeguards for placing the system
    back in operation.

          Our ability to start up the scrubber system and initiate full
S02 removal in the dual stage prototype was further improved by the
completion of the sludge stabilizer addition system.   We had been re-
luctant to add large quantities of lime to the single stage scrubbers,
and equally reluctant to begin operation of the dual  stage scrubber,
both of which result in the production of considerable amounts of
sulfate sludge, without the capability of adding a stabilizer.

SECOND START-UP OPERATION

          Removal of the Coroline material from the dual stage scrubber
fan No. 1 was completed, and startup of the scrubber system once again
began March 17, 1974.  At that time, the dual  stage Scrubber Train No. 1,
and Scrubber Train No. 4 were placed in operation with boilers No. 3
and 4 connected to the scrubber system.  Since then there have been
these additional developments:

  1.  Excessive Fly Ash

      The sludge handling system was designed  so that after 30
      days of normal operation with all boilers tied in and
      with the dual stage S02 prototype and two of the three
      single stage scrubbers, the first curing pond should be
      approximately full.  However, after the  first two weeks,
      one pond was completely filled with only two boilers con-
      nected to the scrubber system during the first week and
      three boilers connected to the system during the second
      week.  This means that, with an average  of 120 megawatts
      connected to the scrubber system, we were producing approxi-
      mately 7,000 tons of sludge in a two week period.  Or,
      stated another way, if the entire plant  were connected to
      the scrubber system, we would fill a pond within a week.
      The major factor contributing to this change in capacity
      proved to be an increased fly ash loading of the scrubber
      system.  The sludge disposal system was  based on a 90%
      combined collection efficiency of the mechanical dust
      collectors and electrostatic precipitators.  The transition
      of the new scrubber ductwork to the old  ductwork is such
      that the gas flow pattern of the gases through the pre-
      cipitators proved to be greatly disrupted.  Velocity
      traverse data indicated that laminar gas flow no longer
      exists.  Rough estimates indicated that  the amount of
      particulates leaving the precipitators and entering the
      scrubber system may have trippled.  Additional  details on
      the sludge handling will be covered later.
                                    c-16

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2.  ID Fan Stress

    As part of the continuing investigation to determine the
    conditions of the ID fans, Structural Dynamics Research
    Corporation (SDRC) was engaged to conduct a series of
    strain gage tests to determine the structural stability
    of the fans.  Their tests indicated that the yield
    strength was being exceeded in several portions of the
    fan blades, and that a degree of metal deformation was
    taking place.  After additional strain gage testing,
    SDRC recommended the installation of doubler (reinforcing)
    plates on each of the blades to reduce the stresses to
    acceptable levels.  After actual tests with stressed welded
    specimens in the fan atmosphere, it was also recommended
    that the doubler plates be welded with an Inconel 112 rod,
    rather than the Carpenter 20, 4 NIA or 8 N12 rods pre-
    viously used.  Since the installation is on a fan-by-fan
    basis, so that a spare scrubber train would always be
    available for emergency backup, it is expected that all
    four fans will not be completed until the end of November,
    1974.

3.  ID Fan Attack

    Frequent shut down of the ID fans for inspection revealed that
    significant attack was still taking place.   Despite the addi-
    tion of lime for S02 removal and pH control, a low pH was being
    encountered in the ID fan drains.  This results from additional
    S02 scrubbing occuring with the fan spray system.  In a trial
    installation, caustic was added to the fan spray water.  How-
    ever, an inordinate quantity is required to obtain even a pH
    of 4, and the trial  will  soon be ended.  As another attempt
    to alleviate the attack,  a new type of fog nozzle was installed
    on one of the ID fans in  an attempt to increase the effective-
    ness of spraying.   No evaluation is yet possible.

4.  ID Fan Deposits

    In addition to the cleaning being accomplished by both the
    original  and the new fan  spray systems, it was necessary to
    periodically remove  the  ID fans from service to remove de-
    posits by manual methods.   In recent, weeks,  this phenomenon
    has not required the need  to clean the blades as frequently.
5.   Recycle Pumps

    An unsatisfactory degree of wear (about 30% in three months)
    is being experienced on the recycle pumps to the point where
    pump parts are being diverted from the Elrama scrubber system

                                  C-17

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     to Phillips at such a rapid rate that the stock of installed pumps
     at Elrama will soon be depicted.  Experimental  pump impellers and
     wear rings of three different materials and design will  be installed.

 6.  Thickener Capacity

     Modifications were made to the thickener tank overflows  to increase
     their hydraulic capacity and thus compensate for the increased dust
     loading and provide spare capacity.

 7.  Throat Dampers

     Significant unacceptable accumulations are still being found in and
     around the scrubber throat damper operating mechanisms.   These have
     restricted the damper operation and  resulted in operation at pressure
     drops of up to 10 inches instead of  the normal  6 inch drop.   Cleaning
     requires removal  of the train from service for manual removal of the
     mechanism and hand cleaning.  About  288 manhours per scrubber are
     required.

 8.  Sump Pumps

     The ID fan spray sump pumps have been wearing out much faster than
     anticipated.  This is due in part to the low pH and to the higher
     solids concentration in the fan drains.  Once again, we  have had to
     draw on the Elrama installation for  replacements.

 9.  Closed Loop Operation

     A closed-loop system may be possible at maximum load with all boilers
     cut-in.  However, the Phillips Power Station is not a base load station,
     and as a result,  the load fluctuates between 30% and full load.  At the
     lower loads, less water is evaporated from the system, while many of the
     points of water addition (purge, seal and spray water) continue.  This
     results in an excess of water in the system.  Temporary  permission was
     obtained from the Pennsylvania Department of Environmental Resources
     (PDER) to discharge the excess to our existing bottom-ash settling ponds.
     This permits the settling out of particulate matter and  dilution of the
     blowdown prior to discharge to the river.

10.  SOg Guarantee Performance Tests

     In July, 1974, several tests were made on the dual stage prototype scrubber
     for S02 removal,  with inlet S02 concentrations ranging from 1263 ppm vol.
     to 1,603 ppm. at stoichiometric ratios from 1.01 to 1.15  the S02 removal
     ranged from 86% to 93%.  The guaranteed S02 removal is  80%.

SLUDGE TREATMENT & DISPOSAL

     At the time the present period of operation started, the sludge
     additive system had been completed to the point where it was
     considered operable.  However, it soon developed that the pumping
     system for the additive was operating below design capacity.  The


                                     c-18

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necessitated pumping a slurry with higher solids content,
and the 750 ft. long transfer lines were frequently out of
service due to plugging.

  This stabilization additive chosen for use is Calcilox,
a proprietary product of the Dravo Corporation.  This
material was developed in the approximate period of
October through December, 1972, when we re-installed the
Chemico pilot scrubber for the sole purpose of making
sludge.  Industry knowledge of sulfate-containing scrubber
sludge and means of stabilization appeared almost totally
lacking at that time.  The scrubber was connected so it
could be supplied from either upstream or downstream of
the existing dust collectors of the No. 4 boiler to enable
experiments with both clean and dirty gas.  The material
developed, Calcilox, is of the consistency of dry cement and,
on the basis of laboratory tests, has the property of con-
solidating the sludge so that it can be disposed of as land
fill without an objectionable leachate.  The degree and time
of consolidation depends on the amount added (3-15% by dry
weight of sludge), the pH of the sludge (10.5 appears suit-
able for our curing time), and temperature (lower temperatures
slow the process).  Since actual field leaching tests had not
been made, we installed two membrane-lined ponds in an inactive
ash disposal area to enable collection and retention of leachate
from Calcilox-treated sludge.  Bottom drain systems were pro-
vided with valves to enable leachate sampling at intervals.
One of the ponds has 22,860 yd3 capacity, the other 5720 yd3.
These capacities may be increased by 502 if the material proves
suitable for successive layering and compacting.

  During the previously noted difficulties with the additive
system, Calcilox was either added sporadically or not added
at all.  As a result, the sludge after residence time in the
ponds was of a "soupy" nature, which made it difficult to
excavate with a clam shell and to transport in open trucks.
Prior to placing the material in the trucks, fly ash from the
ash silo was deposited in the rear of the truck to seal the
tailgate.  Because of the difficulties in handling the sludge,
additional boilers could not be connected to the scrubber
system since it would tax our ability to remove the sludge
from the ponds as rapidly as it was being produced.  Since
the sludge did not have the amount of additive which would
normally be added prior to discharging it to the ponds, no
appreciable degree of stabilization took place in the ponds.
We did not feel that the "soupy" material was representative
of that which would result fron the normal sludge disposal
system, and were reluctant to use one of the lined test
ponds for this material.  Therefore, we requested interim
permission from the State's Solid Waste Disposal Division
of the PDER to dispose of the material on the ash disposal
area where we normally dispose of the fly ash and bottom

                             C-19

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from the generating plant.  The ^tote consented to our
request, and v/e started disposal r,f the unstabilized sludge
on our ash disposal site.  It was spread in thin layers,
mixed with additional fly ash and then compacted.

  Handling of the sludge was extremely difficult.  The trucks
could only be loaded to approximately 1 '2 cepacity because
of the danger of the sludge flowing over the sides if the
truck stopped or started too abruptly or made turns at
excessive speed.  In adJition, because- it was impossible to
prevent sludge from dripping onto the si deb of the truck
during the truck loading operations, it was necessary that
the trucks he washed prior to leaving the plant premises.
Even with such precautions, occasions arose when sludge was
deposited on the roadways.  After several warnings from the
local police and the Pennsylvania Pepartmont of Transportation,
it was necessary to rent a street cleaner and a water sprinkler
truck to clean the streets during the hours of sludge hauling.

  In approximately May, 1974, modifications were completed on
the additive system, and CalcT.ox was then added on a continu-
ous basis to the sludge with dround-the-clcck technical super-
vision.   Filling time per ponri was about- 10-14 days with the
increased quantity of fly ash, instead of the 28-30 days which
had been planned.  Similarly, the curing time was reduced from
30-60 days to 14.  However, v/ith about 107, Calcilox addition
the sludge did consolidate to the extent that drag-line ex-
cavation was possible, truck tailgates did not require sealing,
and it was possible to fully load the trucks.  Observations
of the sludge during excavation showed that although the top
layer resembled hard cloy in consistency, it became earth-like
and then almost fluid near the Lot ton..  It was necessary to
mix the lower-most layer with dryer matfri.il from the upper
layers to obtain a satisfactory hfindlir.1. quality.

  The consolidated material was trucked to and deposited in
one of the lined areas for leachate Monitoring.  However, the
thixotropic nature of the material was such as to prevent
either level inn or successive layering of truckloads.  It
was necessary to tailgate the sludge and then let it stand
(cure?) for about six more weeks before it could bp leveled,
and dozers and trucks did not get ''huny-up."  This, of course,
slows the disposal process consi.lorahly.

  Our present procedure is to ado consolidated sludge to the
lined area whenever possible.  A* other times, it is mixed
and compacted with dry fly asr- or. the normal disposal area.
We have now been monitoring tl.e hcttom drains from the lined
area at weekly intervals for six weeks.  In that time, the
total dissolved solids (TDS) have varied from an original
                             C-20

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      2203 mg/1 to the present (October 2) 3380 mg/1.   A sample analyzed
      by the PDER on September 22 verified the results on our own
      sample of that same date.  Mo record of total volume of leachate
      has been maintained, and it is realized that this quantity can
      affect the measured IDS appreciably.  Similarly, it is realized
      that the method of disposal by tailgating and our inability to
      level the top of the sludge to a possibly impervious surface
      has also had an effect.

        In addition to the above tests, leachate studies were con-
      ducted on a more closely controlled basis.  About June 1,1974,
      we used a concrete mixture to prepare four sludge mixtures
      with various additives.  The additives were fly ash, 2%
      hydrated lime, 5% hydrated lime and 11% Calcilox.  Each mix
      was then added to a plastic wading pool which had previously
      been fitted with a valved underdrain system for leachate
      sampling.  Since the tests started, we have added water to
      each pool once each week so as to cover the sludge after
      first sampling and draining all water from the  previous week.
      After fourteen weeks, the most meaningful tests are those with
      the 5% lime and the Calcilox.  They show that the total dissolved
      solids (TDS) on the lime test started at 1450 mg/1 and are now
      460 mg/1.  The TDS on the Calcilox started at 3370 and are now
      2000.  Penetrometer readings in that time have  increased to
      2.7 tons/ft^ on the lime and 4.5+ on the Calcilox.  In summary,
      while more salts are leached from the Calcilox  mix, the degree
      of consolidation is higher than that of the lime.

FUTURE OPERATING PLANS

          Due to improvements in the method of sludge treatment and
handling, and due to close control of the thickener tank underflow
operation, it was possible to cut-in a fourth boiler  to the scrubber
system on August 18, 1974.  This increased the capacity connected to the
scrubber system to approximately 180 megawatts.  Our  plan is to operate
the scrubber system with the four boilers for a period of time to deter-
mine the extent of any aggravation of existing problems and the occurrence
of any new problems.  If the problems become intolerable, it may be  neces-
sary to return the scrubber system to a three boiler  operation.  However,
if the problems are not severe, we anticipate the possibility of adding
a 5th boiler to the scrubber system.  We are extremely cautious in our
optimism because of the number of unknowns in the sludge disposal system
such as the following:

  1.  Since the lime feed system is essentially operating at
      maximum capacity, additional boilers will reduce the pH
      in the scrubber system.  We are told that a reduced pH would
      adversely effect the stabilization of the sludge.  However,
      we do not know to what degree it will be affected.  Also,
      if additional boilers are connected to the scrubber system,
                                 c-21

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      the rate of sludge production may not permit optimum stabili-
      zation period which now appear to be greatly in excess of 14
      days.

  2.  With the oncoming cold winter months, it is not known to what
      extent low temperatures will hinder stabilization.

  3.  If additional boilers are connected to the scrubber system,
      and it becomes impossible to optimize stabilization of the
      sludge prior to removing it from the pondc, it may be necessary
      to again seal the tailgates with fly ash prior to loading the
      trucks with sludge.  This would then be conducive to sludge
      material dropping on to the road, freezing and causing com-
      plaints from the local citizens.

          If we can connect five out of the six boilers to the scrubber
system by November JO, 1974, we will begin our ten-month test program
at that time to evaluate the efficiency, reliability, and practicability
of the scrubber system.  A decision would then be made on September 30,
1975, concerning the installation of additional S02 removal equipment
for compliance with the S02 emission limitations.  The number of
additional second stage scrubbers required for compliance with the
regulations will be determined during the ten-month test program, and
this will establish the completion date for installation of all additional
scrubbers.

          In the hope of obtaining higher efficiencies of SOp removal with
the use of lime, Duquesne Light is conducting tests using Thiosorbic lime
(a Drayo development) which is a lime having a concentration of magnesium
oxide in the order of 4 to 6%.  Various tests on pilot scrubber systems
indicate that the higher reactivity of such a lime results in S02 single-
stage removal efficiencies in the 90's.  In preparation for these tests,
one of the single stage scrubbers was isolated along with one of the
thickener tanks.  This isolation was necessary to establish and main-
tain the desired chemistry, since lime slaking capacity is insufficient
to maintain the necessary conditions in all scrubbers and both thickeners.
A test run with Thiosorbic lime was made in September, 1974.  However,
we encountered difficulties in achieving a sufficiently high rate of
utilization of the magnesium oxide.  A few cursory tests under these
conditions indicated S02 removal efficiencies somewhat better than those
with high calcium lime, but also significantly less than anticipated.
The tests were suspended later in September to further evaluate means
of increasing the reactivity and utilization of the Thiosorbic lime.
Resumption is planned for about October 21.

          As of August, 1974, construction on the Elrama scrubber system,
which is essentia^y identical to the Phillips scrubber system, had pro-
gressed to a point where no additional meaningful work could be accom-
plished until the problems with the Phillips scrubbers are resolved.
With the modifications and test programs now being conducted at Phillips,
it is anticipated that solutions to the present problems may progress
to the point where startup of the Elrama scrubber system may be possible
in May, 1975.
                                     C-22

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AVAILABILITY AND RELIABILITY

           The availability of the Phillips  scrubber  system is  meaning-
 less at this point since we have essentially 100% backup.   In  other
 words, there are two spare scrubber trains  which  can be  placed in
 service whenever a problem arises on an  operating train.   The  service
 hours for each train for the period from March  17, 1974  through
 September 30, 1974 are 3430 hours for No. 1  train (dual  stage),
 1678 hours for No. 2 train, 1931 hours for  No.  3  train,  and 2803
 hours for No. 4 train.

           Reliability was built into the design of the system  which
 called for a spare scrubber train enabling  us to  carry almost  full
 station load on three scrubber trains.  In  addition, a degree  of
 reliability is built into each scrubber  train through the  instal-
 lation of spare pumps, thickener capacity and backup electrical con-
 trols.

           We do not view bypassing as the solution to maintaining
 acceptable reliability.   However, we have incorporated a manual type
 bypass into our scrubbing system as the  best approach to avoid the
 serious consequences of scrubber failure.   The  system uses blanking
 plates to redirect the gas flow to the original stacks,  and the
 boilers have to be shut down during the  plate change.  Under normal
 circumstances, this process would consume several days depending on
 the availability of manpower.   There really was no alternative in
 designing a bypass system for our plants.   Mechanical bypass systems
 utilizing a damper arrangement require tight dampers, and  sufficiently
 tight dampers have yet to be developed.   We also  had serious space
 limitations on installation of a mechanical  damper system.

 CAPITAL AMD OPERATING EXPENSES

           As of this date, the scrubber  systems at Phillips and Elrama
 represent a capital investment of approximately $61  million.   It is
 expected that an additional $19 million  will  be required for equip-
 ment necessary to comply with the S02 emission  limitations.  This will
 represent a total investment of $80 million or  approximately $91 per
 kilowatt, exclusive of the cost of any additional sludge disposal facili-
 ties required.

           A recent estimate indicates that  the  annual operating and
 maintenance expenses, including fixed charges,  at Phillips and Elrama
 with full S02 scrubbing will be in excess of $30  million per year,  or
 5.5 mills per kilowatt hour, exclusive of additional sludge disposal
 facilities which will be required for full  S02  removal operation. These
 expenses would represent an increase of  approximately $11  per  ton of
 coal consumed.  Expressed in different terms, these  expenses,  without
 fixed charges, would represent approximately a  50% increase over the
 actual operating and maintenance expenses for 1973.


                                    C-23

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          In an effort, to estimate tl',3 t-'U'i capital and operating
costs that would ultimately be incurred for the scrubber systems at
the Phillips and Elrama Stations, including provision of adequate
sludge disposal facilities for full S02 removal, a preliminary
evaluation was made of the additional properfy required for develop-
ment into a disposal area and the additional expenses involved in
disposing of the sludge.  This estimate ii\'itares possible capital
expenditures of $110 million for scrubber  insiallation and property
acquisition and development, of which 551 mi Hi or* has thus far been
spent.  This represents an investment of approximately $124 per kw.

          Present estimates of the sludge disposal costs are $7 to
$10 per wet ton, or $15 to $20 per dry ton of sludge.

Future Objectives

          Although we feel vie ray be able to overcome the present oper-
ating and equipment problem' with ad'J'tion'il time, effort and expense,
there are five levels of performance which must be satisfactorily re-
solved if this flue gas desulfurization syrtem is to be operationally
feasible and economically acceptable:

  1.  Reliability - meaning me scrubber ^arility snould meet
      the degree of availabi'ity nonr-.l:y e/pected of power
      generating equipment.

  2.  Turndown - the capability of the flue ga? desulfurization
      equipment to follow the normal cycling operation of a
      power generation facility without series disruption to
      both the scrubber system and the qoneivfing plant.

  3.  Closed Loop Operation - the ability :,i ~,rvr,ite without
      the discharge of objectionable li^ui:; Affluents as
      dictated by the applicable water quality requirements.

  4.  Sludge - the technique for disposing of sludge from the
      flue gas desulfurization system >«/itliout any adverse
      ecological effects.

  5.  Cost consideration - capital and o>-- Bating expenses should
      not be of such a magnitude as \e unreasonable
      financial burden on the operator/ owner and the consumer.

          Until all these areas of concern are resolved, our system
cannot be considered a successful operation as reports by others have
indicated.
                                    c-24

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                    CALCILOX  CALUL.OX
                    BLPG.    SILO
                                    ELECTBiCAl.
                                    SWlTCHGtzAR
                                      BLDG.
AIR  POLLUTION CONTROL  EQUIPMENT  LAYOUT
            PHILLIPS  POWER   STATION

-------
  HOT FLUE 64S 71? /If
    /£/" STAGS NO 3 I f£CYCLE
    >ymt,(-No4 \  *efo
__ --VJtw) SCRUBUL-R. HO 1
_ «U/M
          HO 3
,/Vd 3MIS.T ELIM
,NO 4 Miyr ELIM

fl ItAIMKTOI?


!
FUEL COMB
OIL. AIR F
\ \

IA/t^f CrA
-------
          DUAL STAG* SCRUBBER TRAIN-PHILLIPS  POWER STATION
HOT FI nc r;/\s
                           COLD FLUE GAS
                                                FUEL  COMRUSTION
                                                OIL.    A IK
                    i	r

-------
                        8ULL MOZZLE;
                          SPRA)
TANGENTIAL NOZZLES
   V
ADJUSTABLE THR.OAT
     PAMPERS
                              LOWER CONE
                      RECYCLE PUMP
                        SUCT/ON
                                            in
 VZNTUZI  SCRUBBER  SECTION
              FIGURE 4 C-28

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                             SIGNIFICANT  DATES
December, 1969


September, 1970
October, 1970


February-May, 1971 -


May, 1971

July, 1971



December, 1971


July, 1973
July 9, 1973


October 8, 1973

March 17, 1974

August 26, 1974

October, 1974
Gibbs & Hill, Inc.  requested to study methods
of compliance.

Gibbs & Hill  study recommends scrubber and
Duquesne Light Company gave authority to
Gibbs & Hill  to proceed with projects at
Elrama and Phillips Power Station.

Invitations were extended to bid on  scrubber
pilot plant.

Chemico pilot scrubber tests at Phillips  under-
way.

Des-ign of full  scale system started.

Contract for scrubber process including scrubber
recycle pumps,  reheater and associated controls
and instrumentation awarded to Chemico.

Construction started at both Phillips and Elrama
plant sites.

Construction of Phase I at Phillips  essentially
complete.  Phase I  consists of one dual stage
S02 scrubber train  and 3 single stage particuldte
scrubber train with associated lime  and thickener
equipment.

Operation began at  Phillips with two and  eventually
three of station's  six boilers.

Scrubber system shutdown for extensive repair.

Scrubber system began with three of  six boilers.

Fourth boiler cut into scrubber system.

Fifth boiler cut into scrubber system.
                                      Figure 5

                                        C-29

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                                 TECHNICAL RCPORT DATA
                              r\ ,7i7 litiinir!i
-------