EPA-660/2-75-020
JUNE 1975
                       Environmental Protection  Technology Series
Refinery Effluent Water Treatment
Plant Using Activated  Carbon
                                    National Environmental Research Center
                                     Office of Research and Development
                                     U.S. Environmental Protection Agency

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                      RESEARCH REPORTING SERIES
Research reports of the Office of Research and Development,
U.S. Environmental Protection Agency, have been grouped into
five series.  These five broad categories were established to
facilitate further development and application of environmental
technology.  Elimination of traditional grouping was consciously
planned to foster technology transfer and a maximum interface in
related fields.  The five series are:

          1.   Environmental Health Effects Research
          2.   Environmental Protection Technology
          3.   Ecological Research
          4.   Environmental Monitoring
          5.   Socioeconomic Environmental Studies

This report has been assigned to the ENVIRONMENTAL PROTECTION
TECHNOLOGY STUDIES series.  This series describes research
performed to develop and demonstrate instrumentation, equipment
and methodology to repair or prevent environmental degradation from
point and non-point sources of pollution.  This work provides the
new or improved technology required for the control and treatment
of pollution sources to meet environmental quality standards.

                         EPA REVIEW NOTICE

This report has been reviewed by the Office of Research and
Development, EPA, and approved for publication.  Approval  does
not signify that the contents necessarily reflect the views and
policies of the Environmental Protection Agency, nor does mention
of trade names or commercial products constitute endorsement or
recommendation for use.

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                                                                          V'
                                     EPA-660/2-75-020
                                     JUNE 1975
              REFINERY EFFLUENT WATER

               TREATMENT PLANT USING

                 ACTIVATED CARBON
                        By

                   Gary C. Loop
                Grant No. 12050 GTR
              Program Element 1BB036
                ROAP 21AZP/Task 027
                  Project Officer

                   Leon H. Myers
Robert S. Kerr Environmental Research Laboratory
     National  Environmental Research  Center
                  P.  0. Box 1198
               Ada,  Oklahoma  74820

     NATIONAL  ENVIRONMENTAL RESEARCH  CENTER
       OFFICE  OF RESEARCH AND DEVELOPMENT
      U.S. ENVIRONMENTAL PROTECTION AGENCY
             CORVALLIS, OREGON 97330
         For sale by the Superintendent of Documents, U.S. Government
               Printing Office, Washington, D.C.  20402

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                               ABSTRACT

Reduction of Chemical Oxygen Demand (COD) in petroleum refinery effluent
wastewater by adsorption onto activated carbon was demonstrated on
a commercial level during a two-year project at Carson, California.
The plant contained over 750,000 pounds of carbon, regenerated
1,644,000 pounds of carbon, processed 172 million gallons of water,
and removed 408,000 pounds of COD.
The carbon was exhausted at the rate of 9.5 pounds per 1000 gallons
of water processed.  At an average feed COD concentration of 250 ppm
and an average effluent COD concentration of 50 ppm, the carbon was
loaded to an average of 0.26 pounds of COD per pound of carbon.
Following solution of initial startup problems, the unit was operated
at a cost of 40 cents per 1000 gallons of water treated, or 18 cents
per pound of COD removed.
This report was submitted in fulfillment of EPA Grant No. 12050 GTR,
under the partial sponsorship of the Environmental Protection Agency.
Work was completed by Atlantic Richfield Company, Carson, California,
January 1974.
                                  ii

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                                CONTENTS


Section                                                       Page

 I       Conclusions                                           1

 II      Recommendations                                       2

 III     Introduction                                          3

 IV      Process Description                                   6

 V       Description of Activated Carbon Plant                 8

 VI      Design Basis                                          20

 VII     Operation and Evaluation of Water Treatment
         Facilities                                            22

 VIII    Operation and Evaluation of Regeneration
         Facilities                                            57

 IX      Test Methods and Their Evaluation                     63

 X       Quantities and Costs Based on Conditions
         During the Project                                    70

 XI      Appendices                                            73
                                  iii

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FIGURES
1
2
3
4
5
6
7
8
9
10
11
12
13
14
15
16
17
18
19
CARBON ADSORPTION PLANT FLOW DIAGRAM
OVERALL VIEW OF CARBON PLANT
IMPOUNDING RESERVOIR
WATER TREATMENT UNIT
VIEW INTO AN ADSORBER CELL
CARBON STORAGE TANKS
CARBON REGENERATION FURNACE AND GAS SCRUBBER
CARBON REGENERATION FURNACE
CAUSTIC TREATING TEST RUN
RELATIVE EFFICIENCY PROFILE OF CELL NO. 3 AFTER
208 HOURS <§ 250 GPM AND 650 TO 600 PPM COD IN FEED
CELL NO. 3 COD VS. TIME FIRST RAINS
FEED AND EFFLUENT COD DATA, FIRST RAINS
COD LOADING, FIRST RAINY PERIOD, CELL NO. 1
COD LOADING, FIRST RAINY PERIOD, CELL NO. 2
COD LOADING, FIRST RAINY PERIOD, CELL NO. 3
COD LOADING, FIRST RAINY PERIOD, CELL NO. 4
COD LOADING, FIRST RAINY PERIOD, CELL NOS. 5
AND 7 THROUGH 12
COD LOADING, FIRST RAINY PERIOD, CELL NO. 6
TWO-STAGE SYSTEM
9
10
11
11
13
15
16
18
24
27
28
30
33
34
35
36
37
38
39
  iv

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                         FIGURES (CONT'D.)



                                                             Page

20     COD CONCENTRATIONS, TWO-STAGE TEST RUN                 41

21     CARBON LOADING, TWO-STAGE TEST RUN                     42

22     FIVE-CELL STAGGERED OPERATION TEST RUN                 47

23     SECOND RAINS RECYCLE OPERATION                         48

24     ADSORPTION DATA, SECOND RAINS, CELL 1                  50

25     ADSORPTION DATA, SECOND RAINS, CELL 3                  51

26     ADSORPTION DATA, SECOND RAINS, CELL 5                  52

27     ADSORPTION DATA, SECOND RAINS, CELL 7                  53

28     ADSORPTION DATA, SECOND RAINS, CELL 9                  54

29     ADSORPTION DATA, SECOND RAINS, CELLS 2, 4, 6, 8        55
       10, 12, 11

30     FURNACE OPERATION                                      61

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                                TABLES
                                                              Page
 1      COD DATA BEFORE AND AFTER VIGOROUS BACKWASHING         25
        AT 5000 GPM

 2      LABORATORY DATA ON CARBON PLANT FEED AND EFFLUENT      31

 3      ESTIMATE OF MAXIMUM WATER THROUGHPUT                   46

 4      TIME REQUIRED FOR REGENERATION                         58

 5      DATA FROM CARBON REGENERATION                          60

 6      ACCURACY OF COD TESTING PROCEDURES                     64

 7      COMPARISON OF ABD AND RE TESTS                         67

 8      COMPARISON OF RELATIVE EFFICIENCY TESTS FOR            69
        REGENERATED CARBON

 9      ADSORPTION DATA                                        71

10      COST DATA                                              72
                                   vi

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                             ACKNOWLEDGMENTS
Personnel and facilities at Carson, California were furnished by
Atlantic Richfield Company.
Mr. C. R. Adams, Engineering Manager, and Mr. M. A. Prosche,
Refinery Technology Manager, served as Project Directors, and
provided administrative and technical assistance.
Mr. Gary G. Loop, Associate Process Engineer, provided technical
direction and prepared the final report.
Mr. E. F. Dumas, Refinery Technology Supervisor, and Mr. P. L.
Mehta, Process Design Engineering Supervisor, provided required
technical assistance.
Mr. R. P. Strand, Waste Water Disposal Supervisor, provided
operational guidance of the plant.
Mr. W. P. Ellertson, Analytical Services Supervisor, Mr. G. R.
Meador, Chemical and Lubricants Laboratory Supervisor, and their
staff performed the laboratory tests and provided interpretation
and comparisons of the test results.
The Environmental Protection Agency provided partial financial
support, and Mr. Leon H. Myers, Project Officer, provided neces-
sary guidance.
                                  vii

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                                SECTION I
                               CONCLUSIONS
1.   Reduction of Chemical Oxygen Demand (COD)  content in refinery
     waste water effluent has been demonstrated to be feasible by
     using activated carbon as an adsorbent.
2.   The system performed well in that it demonstrated an ability
     to start up and shut down without delay or difficulty.   This
     gives the process a distinct advantage over biological  units
     for use in handling intermittent rainfall.
3.   During the two-year project the unit was operated at an over-
     all average cost of 49 cents per 1000 gallons of water  treated
     or 24 cents per pound of COD removed from the effluent  waste
     water.  The first year's operational costs were 62 cents per
     1000 gallons of water treated, or 34 cents per pound of COD
     removed.  After improvements over the first year's operation,
     the costs during the second year were reduced to 40 cents per
     1000 gallons of water treated, or 18 cents per pound of COD
     removed.
4.   The plant demonstrated excellent reliability.
5.   The carbon adsorption plant has demonstrated that when  the
     feed COD is controlled to an average of 233 ppm, the plant can
     treat refinery water using 8.5 pounds of carbon per 1000 gal-
     lons treated and reduce the effluent COD to an average  of
     48 ppm with a high level of 95 ppm.

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                               SECTION II
                             RECOMMENDATIONS
This project demonstrated that activated carbon can be used on a
commercial scale to reduce the Chemical Oxygen Demand (COD) con-
centration of petroleum refinery effluent waste waters.  However,
several areas need further investigation.  These are summarized
below.
1.   Further determination of the quantities and types of COD
     materials that do and do not adsorb onto activated carbon.
2.   Determine feasibility of pretreatment to reduce load on
     carbon.
3.   Determine optimum number of stages in adsorption process
     with controlled feed COD concentrations.
Variables to consider when constructing commercial plant:
1.   Be certain that desired effluent COD concentration is attain-
     able for the particular circumstances involved.  This should
     be done by use of a pilot plant representative of the com-
     mercial plant.
2.   The feed COD concentration range should be determined and
     controlled to eliminate surges.  This could be done by re-
     cycling effluent water, or possibly by some pretreatment
     facility.

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                               SECTION III
                              INTRODUCTION
Petroleum refineries are faced with the problem of disposing of
hugh volumes of waste water.  These large amounts of water come
from a wide variety of sources.  These sources include process
water used for heat transfer, wash water, and rain water runoff
which collects oils and chemicals from within the refinery.
In the past, separation of the visible, floatable oils were con-
sidered satisfactory to allow discharge into adjacent waterways.
However, new concern over the ecological balance of our environ-
ment has called this practice into question.  In an effort to
protect our waterways from these harmful discharges, new and
improved technology is needed.
One major pollutant existing in refinery discharge waters is
oxygen demanding material.  Oxygen demand, which refers to the
demand for oxygen by chemicals and oils, lowers the water's
available dissolved oxygen content, a vital need for marine life.
In 1968, the Los Angeles Regional Water Quality Control Board made
a study of the Dominguez Channel in Los Angeles County.  They de-
termined that petroleum and chemical plant discharges were causing
a problem due to their oxygen demand.  The Control Board, in ac-
cordance with these findings, issued a resolution in February 1968,
which limited the total chemical oxygen demand  (COD) from all
industrial discharges into the Channel.  These discharges included
rain water runoff.  The resolution was to be complied with by
February 1971.
                                   3

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Atlantic Richfield Company's Watson Refinery is one of about 16
industrial facilities discharging water into the Dominguez Channel.
As defined by the resolution, the Watson Refinery was limited to
1330 pounds per day of COD in its discharge water to the Channel.
Meeting this requirement meant reducing the COD in its discharge
waters by 95% if the water was discharged to the Channel.
The Watson Refinery, as a taxpayer of Los Angeles County, made an
agreement with the Los Angeles County Sewer District to have its
process waste water handled in the County's primary treatment unit.
However, due to limitations in the County unit, the County was un-
able to handle rain water runoff.  This presented a problem for the
Watson Refinery due to the fact that the rain water collection
facilities were interconnected with the process waste water collec-
tion system.  Therefore, during periods of rainfall; the process
waste water and rain water mixture could not be sent to the sewer
district facilities due to the presence of rain water, nor could
it be sent to the Dominguez Channel due to high COD content of the
process waste water.
To solve this problem a system was needed which would treat all
the process water plus rain water as it was produced, or an im-
pounding plus processing system which would allow large volume im-
pounding during the rain followed by low volume processing.  In
either case, a system was needed which could be started up easily
when rain fell and then shut down when no longer required.  A
biological unit requires continuous feed and thus the conventional
technology of today was not satisfactory.   Therefore, it was
decided to use impounding followed by activated carbon treatment
to adsorb the COD material from the impounded rain diluted process
water.
Construction of the first commercial sized carbon adsorption plant
for treatment of petroleum refinery waste water was completed in

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1971 and contained over one-half million pounds of activated carbon.
This report describes the first two year's operation of the unit
and is submitted in fullfillment of Project Number 12050 GTR under
the sponsorship of the Water Quality Research Division of Applied
Science and Technology of the Environmental Protection Agency.
The specific objectives of the project were:
1.   Determine feasibility of activated carbon as a treatment
     system for storm water runoff and refinery process waters.
2.   Evaluate performance of the system.
3.   Determine operating costs.
4.  Assess reliability of the system.

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                               SECTION IV
                           PROCESS DESCRIPTION
ADSORPTION
Adsorption is defined as physical attraction of molecules onto a
surface, such as the pore struction of activated carbon.  Acti-
vated carbon is carbon that has been processed to obtain surface
areas in the order of 1,000 square meters per gram by penetrating
the particules with molecular size pores.  The total surface area
is essentially unchanged even by grinding the material to a fine
powder, as the surface area of the outside of the particule is
small compared to the pore surface area.
Strong adsorption takes place by capillary effect as the pore size
nears the size of the molecules adsorbed.  Dissolved organics are
generally more strongly adsorbed than inorganic compounds.  Higher
molecular weight compounds generally displace the lower molecular
weight compounds in the pores.  Non-polar compounds are usually
more strongly adsorbed than polar compounds, and they will also
displace the polar materials.  These and other factors, influence
the net adsorption effect under flow condition in a granular acti-
vated carbon bed.
Activated carbon was used during the two-year project to adsorb
organic chemical oxygen demand materials from the impounded rain
water and process water mixture.  Filtrasorb 300, the adsorbent
used for the Watson Carbon adsorption Plant, is an activated car-
bon with granules having an approximate size range of 8 to 30 mesh
made from bituminous coal.  It is made to high hardness standards
                                   6

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to minimize attrition loss in handling, regeneration, and hydraulic
transport.  It has a broad spectrum of pore sizes to meet adsorp-
tion requirements for a braod range of organic molecule sizes.
THERMAL REGENERATION
Filtrasorb 300 is regenerated by selective oxidation of the organic
impurities in the pores.  This is done at high temperatures
(1600°F-1750°F) and with a controlled low oxygen atmosphere in a
multiple hearth furnace.  As the carbon is heated, the more
volatile organic compounds are vaporized.  With further heating
additional organics are pyrolysed.  The remaining organics are
then oxidized selectively by addition of air.  The carbon is then
quenched in water.  Time, temperature, and atmosphere are the
controllable parameters for regeneration.  Free oxygen must be
carefully controlled in the lower hearths of the furnace to avoid
burning up the regenerated carbon.
CHLORINATION
As there is an inorganic COD background level in the total COD,
provision was made for chlorination after adsorption.  Chlorine
can be added to the effluent stream to permit operating the carbon
beds with some breakthrough of organics as chlorine will reduce
organic COD level as well as inorganic.  This provides greater
flexibility in loading the carbon or in handling an unusual COD
load.

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                                SECTION V
                  DESCRIPTION OF ACTIVATED CARBON PLANT
The water treatment facility is made up of four main systems plus
an impounding reservoir.  Figure 1 describes this system.  An
overall view of the adsorption plant is given in Figure 2.
RESERVOIR
The reservoir is a 1.2 million barrel holding basin which impounds
all refinery waste water and rain water runoff when the Los Angeles
County Sewer District will not accept it.  The reservoir is shown
in Figure 3.
WATER TREATMENT CARBON ADSORPTION UNIT
The water treatment unit is shown in Figure 4.  This unit reduces
the organic COD of water impounded in the refinery prior to dis-
charge to the channel.  The water treatment unit consists of
twelve identical adsorber cells, (V-l through V-12), each 12' x
12' x 23' deep.  Each cell originally contained a 13' deep bed
of carbon having a dry weight of approximately 48,700 pounds.
Supporting the carbon bed is a one-foot layer of gravel on top of
a Leopold underdrain system.  The depth of the carbon was altered
in 1972 for reasons discussed later in this report.
Impounded water is delivered to the influent water distribution
trough through a 14" line from the impounding reservoir.  The
water is distributed to any or all of the twelve adsorber cells
(V-l through V-12) by slide gates.   Flow to each cell is regulated
by a handwheel operated slide gate.

                                   8

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                                                                     1
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                   Figure 1.   Carbon Adsorption Plant
                                  Flow Diagram

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Figure 2.  Overall view of Carbon Plant
                  10

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 Figure 3.  Impounding Reservoir
Figure 4.  Water Treatment Unit




          11
                                                  «

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The waste water first hits a splash plate designed to prevent
packing or pocketing of the bed.  A view into an adsorber cell is
shown in Figure 5.  The water level will be above the surface of
the carbon bed, and the level varies depending on flow rate and
pressure drop from solids accumulation on the bed.  The water
passes down through the carbon bed where it collects in the under-
drain system.
The treated water flows through 6" lines from each cell to a 24"
collection header leading to the effluent retention sump (V-15).
Each 6" cell discharge line has a sample point and an air-operated
pinch valve which can be shut during backwashing.
A chlorine-water solution may be injected into the incoming
treated water stream at the inlet to the effluent retention sump
(V-15).  Approximately 15 minutes retention time is allowed for
chlorine contact in this sump.  The chlorinator (X-l) injection
rate is manually adjusted to further reduce the COD content.  The
treated water collected in sump V-15 overflows through a 24"
underground drain through an outfall box to the channel.
BACKWASH
Each carbon bed must be backwashed whenever it will not pass its
share of water flow due to buildup of solids on top of the carbon.
Frequency of backwashing depends on the rate of build-up of solids
on the carbon bed.  A bed is backwashed whenever it will not pass
its share of water flow.  When this occurs, flow from the bed is
stopped by closing the pinch valve on the 6" discharge line.
Treated effluent is pumped (P-2) from the backwash sump (V-20) up
through the bed to expand the bed and flush out accumulated solids.
Surface washers, which spray water from nozzels on a pipe rotating
just above the carbon bed, will enhance this action.  Bed expansion
is affected by flow rate, water temperature, density, organic

                                  12

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Figure 5.  View Into An Adsorber Cell
                 13

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loading, and surface wash action.  The turbid water overflows into
the backwash troughs to the backwash effluent sump (V-16).  From
there it is pumped (P-3) back to the reservoir for settling and
retreating.
CARBON HANDLING SYSTEM
The carbon handling system includes the storage tanks for spent
carbon  (V-18), and regenerated carbon (V-17); plus the pump,
eductor, piping, and controls to move spent carbon from any cell
to tank V-18, and regenerated carbon from V-17 back to any cell.
The storage tanks are shown in Figure 6.
When the carbon in a bed is exhausted, the flow of water is stop-
ped, the spent carbon removed, and the bed refilled .with regen-
erated carbon.  After a backwashing to remove fines and to
stratify and level the bed, the flow of water is restarted.
The spent carbon is removed from the bed as a water slurry through
a valve in the side of the adsorber cell.  The carbon slurry flows
by gravity in a concrete trench to the suction of the spent carbon
transfer pump (P-l).   The carbon slurry is transferred by pump
(P-l) to the spent carbon tank (V-18) where it is stored prior to
regeneration.
Regenerated carbon slurry is transferred by gravity from its
storage tank (V-17) via hose to the proper cell.  Utility water is
added to assist the transfer.
REGENERATION FURNIACE
The regeneration furnace and gas scrubber are shown in Figure 7.
The slurry of spent carbon is delivered from the bottom of its
storage tank (V-18) to the dewatering screw (M-l) at a controlled
rate.  Motive water is provided from the utility system to eductor
J-l.  To maintain a constant carbon delivery rate, the water level
in the spent carbon tank (V-18) is kept constant.  The carbon
                                   14

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Figure 6.  Carbon Storage Tanks
               15

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Figure 7.  Carbon Regeneration Furnace and Gas Scrubber
                         16

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settles out from the slurry in the feed end of the dewatering screw
(M-l) located above the furnace.  The dewatering screw is set at
an angle so that the water drains from the unit counter-current to
the flow of carbon.  The drained carbon discharging into the fur-
nace contains approximately 50% water (wet basis).  Excess water
overflows"from the dewatering screw and is returned to the reser-
voir.  The dewatered carbon flows by gravity from the dewatering
screw to the top hearth of the regeneration furnace.
The regeneration furnace is a 56" I.D., six hearth multiple hearth
unit.  A diagram of the furnace is shown in Figure 8.  It is gas-
fired on two hearths.  Supplemental air and steam are added on two
hearths.  A center shaft rotates arms with teeth which move the
carbon across the hearths and downward through the furnace.  The
burners on the furnace automatically control furnace temperatures
at the desired levels via thermocouple element and controllers.
Steam and air addition rates are manually set.
The afterburner section is separately gas-fired to raise off-gas
temperatures to about 1450°F.  This is required to combust organic
vapors in the furnace exit gas.
The hot gas from the after burner goes through a quencher where it
is cooled by water injection, is pulled through induced draft fan
(K-4) again with water injection for scrubbing, and exits through
an entrainment separator where entrained water and particulate
matter scrubbed out of the off-gases are removed.  The clean flue
gases are exhausted via stack to the atmosphere.  Hot air from the
center shaft is added to the stack to reduce the humidity and
minimize the vapor plume.
Regenerated carbon discharges down a chute from the furnace in
periodic slugs as the rabble arms pass over the drop hole on the
bottom hearth.  This chute has two legs.  Normal carbon flow is
                                  17

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Figure 8.  Carbon Regeneration Furnace




                  18

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vertically into the quench tank (V-19).  Water level in the quench
tank is kept above the "bottom of the chute to prevent air from
being drawn into the furnace.  A trash screen is provided in the
quench tank to protect the eductor.
The 45° leg on the furnace discharge chute is used to bypass the
quench tank in case transfer problems are encountered.  Opening
the dump gate permits hot carbon to drop directly into drums and
allows continued furnace operation.
Water sprays are provided to quench the hot carbon to eliminate
sudden evolution of steam which would upset furnace pressures.
Quenched carbon is educted to the regenerated carbon tank  (V-17)
where it is stored until needed for refilling an adsorber cell.
                                  19

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                               SECTION VI
                              DESIGN BASIS
The volume of carbon in the adsorbers and Its exhaustion rate are
set by the volume of waste water to be treated, the concentration
and types of adsorbable material in the influent, and the per-
missible COD concentration in the effluent water.  Design of the
full scale unit was based on pilot tests performed on diluted
refinery waste water.
The carbon exhaustion rate was difficult to establish from the
pilot plant tests because the influent COD concentration varied
considerably, both above and below the limits expected under
actual operating conditions.  The actual design of the unit was
based on the following criteria:
               30 days per year of rain (maximum)
               300,000 barrels water per rainy day (maximum)
               9,000,000 barrels of water per year (maximum)
               250 ppm COD average influent concentration
               37 ppm COD average effluent concentration
               1 pound of carbon exhausted per 1000 gallons
                 water treated
Based on these criteria, the unit was designed to handle 100,000
barrels of water per day.   Thus, the unit would run 90 days if the
maximum rains were received without having to replace or regenerate
any carbon.   Based on this operation premise, regeneration of all
carbon would be done during the summer,  non-rainy season.

                                  20

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The regenerator furnace was designed to regenerate 8,500 pounds of
carbon per day.  This is equivalent to 11.3 GPM of slurry from
V-18.  The approximate utility consumption, based on design, was
as follows:
           Steam - 1.0 Ib. of steam per Ib. of carbon = 354 Ibs./hr
           Refinery fuel gas (including afterburner   = 3,000 SCFH
                                 21

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                               SECTION VII
         OPERATION AND EVALUATION OF WATER TREATMENT FACILITIES
This section of the report covers the operation and evaluation of
the adsorber cells and backwashing facilities.
FIRST PERIOD OF OPERATION
The first period of operation covers the first year from May 1971,
through June 1972.
Initial Operation
The unit was first started in May 1971.  The purpose was to test
operation of the unit prior to the rainy season.  Test water was
synthesized by mixing high COD process water with service water
and impounding.  Impounded water was fed to cell 3 at the design
rate of 250 GPM.  With a feed COD of 650 ppm, the effluent remained
in the 44-80 ppm range for the 208 hour run.  In addition to the
COD's being above the design level of 37 ppm, the effluent water
was cloudy and had a septic odor.  This condition of the effluent
was believed to be caused by anaerobic bacteria growing on the
carbon.
Caustic Treatment of Carbon Beds
     It was decided to caustic wash four beds in order to kill the
bacteria and improve COD removal efficiency.  The beds were back-
washed with 2% caustic until a pH of 11 broke through the bed
surface.  A white precipitate formed, a sour smelling gas was
evolved, and the wash solution had a yellow color.   The white

                                   22

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precipitate was easily backwashed out, and is believed to have been
a carbonate compound.  The sour gas is believed to have been H S,
and the yellow color is believed to have been hydrocarbons releas-
ed from the carbon and dissolved in the caustic solution.
A test with the four treated cells in parallel with four untreated
cells was run for 21 hours to determine the effect of the caustic
wash.  The results are given in Figure 9.  Although the effluent
COD's were almost identical for the treated and untreated cells,
the treated cells had very little problem with odor and clarity
in the effluent water.
Because of the improved odor and clarity of the water from the
caustic treated cells, all 12 cells were treated.  With continued
operation it was soon apparent that the adsorption plant was not
adsorbing as much as expected,
Backwashing
Since the carbon was not adsorbing the COD in the amounts it had
in pilot plant work, it was felt that trapped air might be de-
creasing the available surface area on the carbon.  In an attempt
to decrease the trapped air, a more vigorous backwash was used for
three cells.  The backwash rate was increased from 3,300 GPM to
5,000 GPM, which resulted in an increased bed expansion from 20%
to 50%.
Although the effluent COD's were temporarily reduced to below
30 ppm, the improvement lasted only one day.  The results from
cell three are shown in Table 1.  Since the increased backwash rate
showed no permanent improvement, it was discontinued.
The frequency of backwashing was studied during the test runs
described below.  In run 4, backwashing was infrequent, while in
run 5 the cells were backwashed daily.  Despite a lower feed rate
and lower feed COD in run 5, both run 5 and run 4 had equal effluent

                                  23

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£30$-
     n
                                                                                                 500
                                                                                              — 400
                                                                                                 300
                                                                        NON-CAUSTIC
                                                                        TREATED CELLS
                                 CAUSTIC  TREATED CELLS
8
     10      12      14
   ELAPSED TIME, HOURS
9 . Caxiatijc. Ti:e.a.tijn.e. Test
16
18
20
22

-------
Table 1.  COD DATA BEFORE AND AFTER VIGOROUS BACKWASHING
                     AT 5000 GPM

                        CELL NO. 3

                    FEED RATE = 250 GPM

J3ATE
9-15-71


9-24-71





J-25-71


>-26-71

TIME
11:00 AM
1:00 PM
3:00 PM
11:45 AM &
For 10 and
3:00 PM
6:00 PM
7:30 PM
11:00 PM
7:00 AM
3:00 PM
11:00 PM
7:00 AM
11:00 PM
FEED ppm EFFLUENT ppm
194
189
264
83
89
114
12:45 PM backwashed @ 5000 GPM
11 minutes respectively
75
—
167
119
119
113
116
181
118

<30
42
53
72
76
74
77
33
76
                           25

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COD's.  Increased frequency of backwashlng is not felt to be an
Improvement for COD removal.
COD Penetration Into Carbon Bed
Cell number three was stopped after 208 hours of operation to study
the problem of high effluent COD.  Besides the testing of caustic
washes and backwashing, data was collected to determine the rela-
tive efficiency at various depths in the carbon bed.  The data is
shown in Figure 10.  The relative efficiency test, which is de-
scribed in Appendix B, is an indication of the carbon's ability to
adsorb COD compared with virgin carbon.  The reliability of the
test is discussed in the "Test Methods and Their Evaluation" sec-
tion of this report.   The data in Figure 10 indicates that the
top two feet of carbon were completely exhausted while the last
five feet were still at 65% of virgin adsorption ability.
Exhaustion Run
Cell three was run for 247 more hours during which time the plant
was stopped once on September 17, 1971, and restarted again on
September 24, 1971.  The results for the last 247 hours are shown
in Figure 11.  During the seven days the plant was down, the feed
COD decreased about 180 ppm.  It appears that natural oxidation
reduced the COD in the impounding reservoir.
Cell three was regenerated when feed and effluent COD's converged
in the 431st hour.  The exhaustion rate could not be calculated be-
cause by design criteria the bed is exhausted when the effluent
COD exceeds 37 ppm.  The effluent was rarely below 40 ppm.  Based
on the entire run, the carbon was used at the rate of seven pounds
of carbon per 1,000 gallons of water treated.
Varying Flow Rates
As rainfall was extremely light, there was very little water pro-
cessed by the carbon plant in the winter of 1971 and 1972.  In
addition to the light rainfall, the sanitation district accepted
                                  26

-------
  z
  LJJ
  •—i
  CJ

  u_
  u_
  LLJ

  LJ.I
ISJ
       0
45678


  DEPTH  DOWN  INTO  CARBON  BED,  FEET
                                                                                                10
                   Figure 10.  Relative Efficiency Profile of  Cell  No.  3 After  208 Hours at 250 GPM

                                                 650 to 600 PPM COD In  Feed

-------
 320
 280
 240
o.
Q.
Q
O
 120
  80
  40
                                    I        I
   200     220     240     260     280     300
320     340


TIME,  HOUR
360     380     400      420     440     460
                                 Figure  11.  Cell Number Three COD Vs Time First Rains

-------
 process waters with COD's above 450 ppm 24 hours after rainfall
 stopped.  Therefore, water was only processed when there was water
 in the impounding reservoir with a COD below 450 ppm.  Throughout
 the winter,  six runs were made with varying flow rates.  Data
 from the six runs is given in Figure 12.
 Run 1
 The carbon plant was started at 4 p.m.  on December 25, 1971, with
 a design feed rate of 3,000 GPM.   All 12  cells were in service.
 The run lasted 44 hours with an average feed COD of 326 ppm and
 an average effluent COD of 43 ppm.   The run was stopped when the
 feed COD jumped above 450 ppm.  During  this run,  samples of feed
 and effluent were tested for COD,  turbidity, color, odor, and
 suspended solids.   The results of  these tests are listed in Table 2.
 Run_2_
 Run 2 was started when the feed COD dropped to 415 ppm.   This run
 which lasted 47.5 hours had an average  feed COD of 360 ppm and an
 average  effluent COD of 48 ppm.  Halfway  through the run,  the rate
 was reduced  to 2,000 GPM to comply  with channel discharge limita-
 tions.
•SyjL_3
 Again 2,000  GPM was  continued  as effluent  COD's average  80 ppm.
 The feed  averaged  374 ppm and  the run lasted 38.5 hours.
J*un_4_
 The  fourth run lasted only 18  hours with a  feed rate  of  2,000 GPM.
 The  average  feed COD  was  310 ppm and the effluent averaged  67  ppm.
|un_5_
The  effluent was still well above 37 ppm COD with an  average  COD
°f  66 ppm.   The  feed  rate was  cut to 1,000 GPM  to assure com-
pliance with the COD  discharge limitation.   The feed  averaged
                                  29

-------
900 —
800 —
                                                                                    1-RUN 6-|
         20
40
60
80
100   120    140
 TIME , HOURS
160
180
200   220   240   260   280
                       "Figure 12.  "Feed and Effluent COD Data "First Rains

-------
         Table 2.  LABORATORY DATA ON CARBON PLANT FEED AND EFFLUENT
Date
•*••*• !•! 1
12-27-71
12-28-71
12-29-71
Effluent
12-27-71
12-28-71
12-29-71
COD
690
415
370

43
15
40
Turbidity
J.T.U.
56
41
36

14
14
12
Color
65
72
60

11
15
13
Odor
8
8
12

1
1
1
Total Suspended
Solids, ppm
122
64
132

11
20
34
 237 ppm COD  if  the  extremely high peak  in Figure 12 of 900 ppm COD
 is discredited.  This was  the  longest of the six runs and lasted
 95 hours.
Run six lasted 22 hours with an average feed COD of 147 ppm.  Al-
though the feed COD was low, it had a green algae which was not
adsorbed or filtered by the carbon bed.  The effluent which
averaged 93 ppm COD was also green in color.  The problem with
algae occurred again during later testing and is discussed under
the "Two-State Test Run" heading of this section.
^valuation of First Rain's Operation
        several attempts to improve operation, the carbon adsorp-
tion plant was unable to process water at the design rate of
100,000 barrels per day, and still meet county regulations.  Fort-
unately, rains were light, and the sanitation district accepted
high COD water.
                                  31

-------
The COD loadings of each cell vs. gallons of water treated are
given in Figures 13 through 18.  The loadings varied from 0.2 pounds
of COD per pound of carbon to about 0.3, at the end of the first
rainy season.  Since the effluent COD's remained about 37 ppm, a
precise determination of COD loadings at breakthrough is not
possible.  Therefore, an estimate was made in September, 1972 as
follows:
  Feed              Loading              Carbon Exhaustion Rate
COD, ppm     Lbs. COD/Lb. Carbon   Lbs. of Carbon/1,000 Gals. Treated
  150              0.35                            3
  250              0.30                            6
This estimate is based on the assumption that the beds are extreme-
ly sensitive to surges of COD.  The surges may penetrate deep into
the bed and prevent the necessary COD removal in the low range.
Since rainfall was light, dilution of the COD with rain water was
greatly decreased.  The result was extremely erratic feed COD con-
centrations and poor carbon plant operation.  It should be empha-
sized, however, that the estimates are based on assumptions which
have not been validated and the estimated loadings have never
been achieved prior to breakthrough.
TWO-STAGE TEST RUN
The data in Figure 10 shows that the carbon near the top of the
bed adsorbs much more COD than the lower portion of the bed.  There-
fore, if the bed could be cut in half, only the more heavily
loaded top portion would need to be regenerated.  This would allow
a much higher COD loading.   Since an individual cell cannot be
split in half, a system was devised to test two cells in series.
Description of System and Operation
Cells number two, six, and seven were used in a two-stage test run
from July 12, 1972, through August 30, 1972.  Both phases of the
downflow upflow system are shown in Figure 19.  In order to
                                  32

-------
CO

u>
       a
       o
       CD


       o

       o
       o
       CO
       a:
           0
                                         FIGURE 13


                                        COD  LOADING


                                    FIRST  RAINY PERIOD


                                        CELL NO,  1
  1000               2000              3000


VOLUME  OF WATER TREATED,  THOUSANDS  OF GALLONS
4000
                        Figure 13.  COD Loading First Rainy Period Cell No. 1

-------
     o
     m
     a:
     <
     o
Co
     O
     <
     O
     O
     CQ
     QC
                                                                                o
                                                                                LU
                                                                                LU
                                                                                o;
          0
1000
2000
3000
4000
                                 VOLUME OF WATER TREATED, THOUSANDS OF GALLONS


                                         14.   COB l^oaditig ¥lrst Rainy Period Cell No. 2
_J

 5000

-------
       .30
    z
    o
    CQ
    OC
    <
    O
       .20
LO
     Q
     O
     CJ
       .10
     O
     PQ
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                                                                          UJ
                                                                          o:
                                                                          UJ


                                                                          ill
                                                                          CJ3
                                                                          UJ
                                                                          Of-
2000
3000
4000
6000
10000
                                  VOLUME  OF WATER TREATED, THOUSANDS  OF GALLONS
                                    Figure  15.  COD Loading First  Rainy Period Cell No.  3

-------
  1000               2000              3000
VOLUME  OF WATER  TREATED, THOUSANDS OF  GALLONS

  Figure 16.  COD Loadings First Rainy Period Cell No. 4
4000

-------
                                                     COD LOADING
O
PQ
O
                                                 FIRST  RAINY PERIOD


                                          CELL NOS,  5 AND NO, 7 THROUGH 12
      0
1000
2000
3000
4000
                              VOLUME  OF WATER TREATED, THOUSANDS  OF GALLONS
                             Figure 17.   COD Loading First Rainy Period Cell Nos. 5

                                            and  No. 7 through 12

-------
CD
        CQ
             o
             3
             <
        o
        CQ
        OL
     0.20
            oq
O
u
      0.10
        0
                                               1
                                                      1
                           1000
      2000               3000                4000

VOLUME OF WATER TREATED THOUSANDS  OF GALLONS


 Figure 18.  COD L.oadin.g, ¥irst Rainy Period Cell 15o. 6
                                                                                         '3000

-------
                        PHASE  1  OF  TWO  STAGE  SYSTEM
•MTER FROM
RESERVOIR




1
STAGE
1
CELL
2





TO CHANNEL
I
STAGE
2
CELL
6








CELL
7
- ^




* t
                       PHASE  II  OF  TWO  STAGE  SYSTEM
'/ATER FROM  RESERVOIR
TO CHANNEL








CELL
2





J
STAGE
1
CELL
6





!
STAOE
2
CELL
7
	 ».




4 t
                    Figure 19.   Two  Stage  System
                                39

-------
increase the adsorptive capacity of the unit, 15,000 pounds of
carbon were added to the existing 48,700 pounds in each of the
cells used.  This increased the bed depths from 13 feet to 17 feet
to give a total of 63,700 pounds in each cell.  The first phase
used cell number two as the first stage with downflow, and cell six
as the second stage with upflow.  At the beginning of the second
phase, cell number two was taken out of service, cell number six
became stage one -with downflow, and cell number seven was placed
in service as the second stage with upflow.  Since no rain fell
during the summer, the feedwater was made up in the impounding
reservoir every two or three days using several water sources in
an attempt to maintain the COD concentration at 250 ppm.
The feed rate to each cell during the first phase of the test run
was held constant at 500 GPM.   This is equivalent to the design
rate of 3,000 GPM for the entire plant.  The feed rate was reduced
to 250 GPM for most of the second phase to see if a lower effluent
COD could be reached.
Results
The results of the two-stage run are shown in Figures 20 and 21.
Figure 20 shows the COD concentrations of the feed, first stage
effluent and second stage effluent as a function of gallons of
water processed in the unit.  Figure 21 shows the COD loading of
each cell vs. gallons of water processed.  At the end of Phase 1,
the first stage had a loading of 0.39 pounds of COD per pound of
carbon and the second stage had a loading of 0.11.  The effluent
COD at the end of Phase 1 was well above the desired 37 ppm.
There was also a problem with algae growth, which, as discussed
later in this section, was adversely affecting the test run re-
sults.  Since lower COD effluents were not detected during Phase 2
and because the unit had to be readied for the next rainy season,
the run was terminated.  As can be seen in Figure 20, the effluent
remained below 100 ppm virtually the entire run.
                                  40

-------
400
          2000    4000
6000   8000-   10000   12000   140QO   16000   18000   20000   22000
          VOLUME OF  WATER TREATED,  THOUSANDS OF GALLONS
2*000  26000   28000
                                    Figure 20.   COD Concentrations  Two-Stage Test Run

-------
S.30[
CL.
<
O
9
o
o
 J.20
a
<
o
o
OQ
  . 10
                                         FIGURE 21



                          CARBON LOADING TWO-STAGE TEST RUN
                             CELL-2
                       STAGE 1
          2000
4000
6000
8000   10000   12000    14000   16000   18000   20000   22000

VOLUME OF WATER TREATED, THOUSANDS OF GALLONS
                                                                                                   26000  28000
                                  Figure 21.  Carbon Loading Two-Stage Test Run

-------
 Validity of Results
 By the definition used for the Watson Carbon Plant,  the carbon is
 considered loaded when it contains so much COD that  its adsorption
 capability is  reduced to the point where it cannot adsorb enough
 COD to keep the effluent below 37  ppm.   Ideally,  this  loading  could
 be determined  by running the carbon plant under the  expected rainy
 season conditions until the effluent becomes greater than 37 ppm,
 Or>  in other words, until "breakthrough" occurs.   Unfortunately,
 the  system cannot be  operated  at a steady feed  concentration of
 250  ppm COD until there is enough  rainfall to dilute the  COD to
 250  ppm.   The  COD during test  runs could not be kept at the desired
 concentration  on a day  to day  basis  because  it  takes several hours
 to determine the COD,  and thus,  any concentration  surge would be
 detected too late.  Therefore,  an  estimate of operation under  ideal
 conditions  free  of surges  and  algae was made for  the two-stage
 system as was  previously done  for  the single stage system.  This
 estimate is  that  the  two-stage  system can  load  to 0.39 pounds of
 COD per pound  of  carbon.   This  is  the same as attained by the
 first stage during Phase  1 of  the  test run.
      Growth
      growth in the water  impounding reservoir first appeared at
 the end of the first rainy season.   The algae was  easily identified
as it gave the water a green coloration.  The carbon adsorption
Plant was adversely affected by the algae as indicated in run six
Curing the first rains.  During this test run, the carbon plant
had one of the lowest average feed  COD concentrations (147 ppm)
tested, and yet, due to the presence of algae, the effluent averaged
93 ppm COD.
*he algae problem appeared again in July 18 in the water fed dur-
    the two-stage test run.  A study of reservoir  algae control
                                 43

-------
revealed that algae growth can be kept low by use of small concen-
trations of copper sulfate.  On July 28, solid copper sulfate was
spread over the surface of the reservoir to give a content of about
0.0002 weight percent.  Within 72 hours the algae was greatly re-
duced.  Since the effect of the CuSO, is not permanent and no more
addition of CuSO  was made, the algae became so concentrated that
the carbon plant had to be shut down on August 18.  Copper sulfate
was again spread over the reservoir on August 22 to reduce the
algae.  Three days later it was added again which kept the algae
at low levels until the end of the two stage test run.
Since the algae problem was never experienced again, no further
investigation was made into its control.
Evaluation of Two-Stage System
The one-stage system can load to an estimated 0.30 while the two-
stage system can load to an estimated 0.39.  This gives the two-
stage system a distinct advantage over the previous single stage
operation.  The two-stage system also has the advantage that it
ran longer than any test run and had one of the lowest average
effluent COD concentrations (47 ppm).  It should be re-emphasized,
however, that the predicted loadings of the carbon used for com-
parison have never actually been achieved prior to breakthrough.
SECOND RAINY PERIOD
Single Stage System
Although plans called for converting the carbon plant to a two-
stage system if it proved superior, a change in Los Angeles
County sanitation regulations allowed rain diluted waste water to
be pumped to the sewer.  Previously, only limited quantities of
impounded water were permitted, and then only if COD was above
450 ppm.  The plant was used as a single stage system to process
impounded water from October 1972, through July 1973, since
pumping limitations prevented discharging all impounded water to
the sewer.
                                  44

-------
 The  12  carbon cells  were divided  into  two  groups:   (1)  those  for
 testing purposes;  and  (2)  those for  handling  the bulk rain water.
 To allow the  accumulation of  additional  data  under  controlled
 conditions  relative  to  alternative modes of operation,  five of  the
 cells were  designated for  use only for testing purpose.  The  re-
 maining seven were designated for use  in processing the bulk  rain
 Water as it was  impounded.
 .Staggered Mode Operation Test Run
 The  choice  of five cells for  test purposes is based on  the calcu-
 lations shown in Table  3.  These calculations were  used to estimate
 the maximum number of cells which could  be operated continulusly
 based on predicted plant limitations.  The calculation  is simply a
 determination of how much water can  be processed to load carbon at
 the  same rate it can be  regenerated.   A  staggered operation was
 devised to  allow three  cells  to operate  at all times without  delay
 for  regeneration.  In order to start the test run,  it was neces-
 sary to start one  cell each week.  At  the end of three weeks, a
 fourth  cell was  started  while the first  cell was moved to the
 spent carbon  tank  and regenerated.  At the end of the fourth week,
 the first cell had been  regenerated and was ready for use.  However,
 a fifth cell was used and the first was put on stand-by to be used
 at the  end of  the  fifth week.  The extra fifth cell was used as a
 buffer  against temporary mechanical holdups.   The mode of operation
 is shown in Figure 22.
 Since the impounding reservoir had a high COD content, effluent
Water was recycled back  to dilute the feed as is shown in Figure 23.
 The total feed rate  to each cell, which includes the recycle was
maintained at  250  GPM while the unit was in operation.  Air was
 dispersed into the effluent sump to kill anerobic bacteria that
might be recycled  to the beds.
                                  45

-------
             Table 3.  ESTIMATE OF MAXIMUM WATER THROUGHPUT


Estimated Feed COD                            300 ppm

Estimated Loading                             .30 Lb. COD/Lb. Carbon

Estimated Carbon Regeneration Ability         9,000 Lb. Carbon/Day

Estimated Effluent COD                        30 ppm
8.34 x 10 6  	Lb. COD	.  (300 ppm - 30 ppm)  =
             (Gal. H20)(ppm COD)
                                 2.252 x 10~10   Lb. COD
                                                (Gal. H20)
9,000 Lb. Carbon/Day (.30 Lb. COD/Lb. Carbon)  =  2,700 Lb. COD/Day
       2,700 Lb. COD/Day
2.252 x 10-3 Lb. COD/(Gal. H20)  24 Hrs./D  60 M/Hrs.  =  833 GPM
With a feed rate to each cell of 250 gpm, 3 cells were used for a

total of 750 gpm.
                                   46

-------
TWO
THREE
FOUR
FIVE
SIX
FIRST
CELL
LN
USE

IM
USE

I • v
USE

REGEN.

STAND
3Y

IN
USE












SECOND
CELL


in
USE

IN
USE

IN
USE

REG EN.

STA'!:')
3Y












THIR:)
CELL




IN
USE

IN
USE

IN
USE

REGEr!.












FOURTH
CELL






IN
USE

IN
USE

IN
USE












FIFTH
CELL 	








IN
USE

IN
USE
                 Figure  22.   Five-Cell  Staggered  Operation Test  Run
                                     47

-------
FRESH FEED
1 "-^ 	 " ••
i



-t*
00




k
1 1
BULK
TEST PROC.
CELLS CELLS
"

EFFLUENT
SUMP
CI2 INJECTION | |
j
                                                                RECYCLE
TO CHANNEL
                                    Figure 23.   Second  Rains  Recycle Operation

-------
The COD concentrations and loadings of each, of the five cells are
plotted in Figures 24 through 28.
After the cells had finished one cycle, it was apparent that the
carbon could not keep the effluent COD below the desired 37 ppm
f°r a full week, despite the dilution of the feed.  Therefore, it
vas decided to chlorinate the effluent in the hope that COD mole-
cules which had not been adsorbed on their first pass through the
b^d might form a halogenated molecule which would be more likely
to be adsorbed.  The chlorine was added at 100 pounds per day for
the remainder of the test.  Since it was difficult to determine
the effects of the chlorine addition, the cells were not switched
as scheduled.  They were run an extra two weeks before it was
decided that there were no noticeable improvements with the
chlorine.
           Bulk Rain Water
    n of the 12 cells were used for processing bulk rain water dur
    the second rainy season.  Bulk rain water refers to water in
    reservoir when the level in the reservoir is high enough to
limit the ability to impound water beyond reasonable expectations.
About 40.6 million gallons of water were processed through the
8even cells.  The influent and effluent COD's along with the
carbon loading are plotted vs. gallons of total water treated in
^igure 29.   The chlorine addition start time is also indicated in
pigure 29.   When the rain season ended, the cells were loaded to
°-3l pounds of COD per pound of carbon.
•Valuation of Second Rainv Period
     g the second rainy period 102,000,000 gallons of water were
Processed.  The average diluted feed COD concentration was 233 ppm
vhile the effluent averaged 48 ppm with a high of 95 ppm.  The
carbon loaded to an average of 0.26 pounds of COD per pound of
      .
                                   49

-------
E
o.
a
o
O
     3OO



     aoo


     100



      o
S

^   0.40
o
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5   O.EOH
a
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te.
    0.10



     0
                       FEED
                 EFFLUENT
                               o
                               ID
                               UJ

                               UJ
                               o
                               Ul
                               a:
                  1
I
           2000 4000  6000 8000    0  2000  4000 6000 8000  10000 12000


                VOLUME OF WATER TREATED, thousands of gallons
                Pigure 24.
                             Adsorption  Data Second  Rains

                                     Cell  1
                                     50

-------
a
Q.
Q
8
   300
   200
   100
 § 0.40
 
-------
   300
   200
o

8   100
o
o
^  0.40
o
o
o
„  0.30
o
5 O.20
o

§
   0.10
z
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t£.
<
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             FEED
       —   EFFLUENT
                             o
                             UJ
                       o
                       Ul
      I
I
I
0   2000 4000  6000 8000   0   2000 4000

       VOLUME  OF WATER TREATED,
         thousands of gallons
        Figure 26.
               Adsorption  Data Second Rains

                       Cell  5
                            52

-------
 E
 a
 a
a
O
o
1
a
u
I
2   0.20 —
5

§
CD
a:

2
300



200




100
    0.40



    030
    0.10 —
                            FEED
                    EFFLUENT
                                              o
                                              uj
                                         (C
                                         IU
                                         z
                                         UJ
                                         o
                                         UJ
                                         or
         I
                   I
I
I
   0  2000 4000  6000 8000 10000 12000  14000

  VOLUME OF WATER TREATED, thousands of gallons
        Figure 27.
                 Adsorption  Data Second  Rains

                           Cell 7
                              53

-------
E
a.
Q.
o
o
o
300




200




100




  0
e
o
O
u
Q

O
O
    0.40
0.30
2
o
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5
<
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o
CD
 r  0.20
0.10
              FEED
               EFFLUENT
                           z
                           UJ
                           o
                           UJ
                           cc
         I
I
I
1
1
       0  2000  4000 6000 8000  10000  12000 14000


      VOLUME OF WATER TREATED, thousands of gallons
          Figure 28.
                   Adsorption Data  Second Rains

                            Cell 9
                              54

-------
                    FEED
 E
 a.
o
o
u
 300



200




 100
                   EFFLUENT
c
o
o
u
o
O
O
    0.40
0.30
                                   o
                                   I
                                   Uf
                                   o
                                   Ul
                                   DC
   0.20-
o
<
3

o
o
oc
    0.10-
            I
              I
I
I
          2000 4000 6000 8000 10000

           VOLUME OF WATER  TREATED,

            thousand! of gallons
        Figure 29.
                 Adsorption Data  Second Rains

                 Cell Nos. 2,4,6,8,10,12,11
                          55

-------
Although the carbon plant was operated without violating the limit
of 1330 pounds per day of COD, a large portion of the impounded
water was not processed in the plant.  The change in county regula-
tions relieved the need for meeting design operation.  The con-
trolled COD level in the feed allowed for the highest average carbon
loading during the two-year project.
The five-cell test run showed that control of the feed COD concen-
tration Improves carbon loading.
                                  56

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                               SECTION VIII
            OPERATION AND EVALUATION OF REGENERATION FACILITIES
 This section of the report covers the operation of the carbon re-
 generation furnace and carbon transfer equipment.
 FIRST PERIOD OF OPERATION
 Twelve cells were regenerated during the first period of operation.
 The time required for regeneration for the first seven cells is
 tabulated in Table 4.   The time includes all downtime for repairs.
 The regenerations vary in time from 4.0 days to 14 days with an
 average of 9.8  days.   The unit was designed to regenerate a bed in
 5.7 days.   The  causes  of  the extended regeneration time are dis-
 cussed below.
.Temperature Excursions
 During the first  regenerations the temperature on  hearths four  and
 six would  fluctuate from  1700°F to 1850°F in 10 to 20 minute cycles.
 Several  attempts  were  made  to  adjust  the  controllers  but  there  was
 no  improvement.   The thermowells were changed from 3/4" standard
wall to  1"  heavy  wall  stainless  steel and the thermocouples  were
 changed  from iron constintan to  chrome alumal.   The temperature
controller  on hearth six was found  in need of  repairs and was
 fixed.   The temperature excursions were reduced  to only 50°F in
future runs.
jj-ductor Weajr
The original design used 1" cast iron eductors and 110 pound per
square inch motive water to transport  carbon to  the furnace  screw
                                  57

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             Table 4.  TIME REQUIRED FOR REGENERATION

TIME REQUIRED
CELL NO.
3 9 AM,
2 2 PM,
6 9 AM,
8 4 PM,
10 3 PM,
12 2 PM,
11 1 AM,


START
Nov. 2,
Feb. 17,
April 19
May 11,
May 26,
June 12,
June 20,


1971
1972
, 1972
1972
1972
1972
1972


10 PM
4 AM,
6 PM,
10 PM
3 PM,
12 N,
3 PM,


FINISH
, Nov. 10
March 1,
April 27
, May 20,
June 9,
June 17,
June 30,


, 1971
1972
, 1972
1972
1972
1972
1972
Total
Average
hours
205
302
201
222
336
118
254
1638
234
days
8.5
12.
8.
9.
14.
4.
10.
68.
9.
6
4
3
0
9
6
HM
3
8
feeder and away from the furnace regenerated carbon quench tank.
The capacity of these eductors when in new condition was about 6.5
pounds of carbon per minute.  Due to erosion of the throat, both
of the eductors lost efficiency after three regenerations.  This
loss of efficiency limited the feed to the furnace.  In addition to
the eductors wearing out, they had many problems with plugging, but
this was alleviated with screens to stop large chunks from entering
the eductors.
High Gas Velocities
A problem with fines blowing out the stack was encountered, but
was alleviated by lowering the steam rate.
                                   58

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 High Shaft Rates
 Due to mechanical problems, the shaft which moves the rabble arms
 over the carbon was rotating at three RPM instead of the design
 rate of 1 RPM.  The rate was reduced to two RPM's after adjustments
 were made.  During the seventh regeneration, the bolt which locks
 the motor drive shaft to the drive gear broke.   This may have been
 due to running the rabble arms above design rate.
 .Evaluation of Furnace Problems During the First Period of Operation
 Most of the problems encountered with the furnace operation were
 mechanical in nature.   Therefore, they could be solved as more
 experience was obtained.

 TWO-STAGE TEST PERIOD
 Operation
 The three cells used in the two-stage test run  were  regenerated
 without stoppage for mechanical  problems.   The  major reason for
 the success was larger  eductors  and  reduced motive water  pressure.
 The 1"  cast iron eductors were replaced with 1  1/2"  stainless
 steel eductors.   The changes allowed the  carbon to be moved without
 Wear or plugging.  The  uninterrupted feed  of carbon  allowed for  a
 steady  operation and the temperature excursion  problem  ceased  to
 exist.   The new eductors allowed  the flow  of carbon  to  go  as high
 as  10 pounds per minute.  The data from the regeneration  is  given
 in  Table  5.  Figure 30  shows a plot  of regenerated carbon  relative
 efficiency  vs.  carbon feed  rate to the regenerator.
^valuation  of Improved  Regeneration
 The larger  eductor is believed to have solved most of the  regener-
 ator problems.
 pigure 30 is based on limited data, and thus,  the accuracy  is
 questionable.   However, the general  trend of decreased quality of
*egenerated carbon with increased feed rate is believed correct.
                                  59

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             Table 5,  DATA FROM CARBON REGENERATION

DATE
September 18
19
20
21
22
23
24
25
26
27
CARBON FEED RATE APPARENT
pounds /min. SPENT
.59
.58
6-6.5 .58

7-7.5
8-8.5
.52
10
.55
.55
DENSITY
REGEN.
.495
.52
.515
.49
.48
.48
.475
.465
.48
.46
RELATIVE EFFICIENCY
SPENT REGEN .


95.8%
94.3%
88.0%
88.0%
64.6% 79.7%
86.5%
27.6% 86.5%
67.7% 85.9%
SECOND RAINY PERIOD
During the second rainy period, regenerations continued with no
problems.  A major portion of the time was spent collecting data
for improving testing techniques which are discussed in detail in
the "Test Methods and Their Evaluation" section of this report.
On April 23, 1973, the APCD tested the regenerator furnace stack
for CO and found the CO content over the allowable concentration of
0.2% by volume.  This forced a shutdown of the furnace.  It was
felt that the insufficient combustion efficiency was caused by the
combustion air damper set nearly closed and a low afterburner
temperature.

                                 60

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96 L
                   7               8                9               10
                       CARBON FE€D RATE TO REGENERATOR FURNACE, LB,/MINUTE
11
                                   Figure 30.  Furnace Operation

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Upon obtaining a test permit the furnace was restarted in October
1973, with the combustion air damper wide open and the temperature
controller increased from 1400°F to 1550°F.  With these changes
the CO is well below pollution concentration.
                                  62

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                                SECTION  IX
                    TEST METHODS AND THEIR EVALUATION
GOD DETERMINATION
There are several means of determining  the chemical oxygen demand
(COD) of a solution.  Three of  these methods, which are described
in Appendix A are EPA HIGH LEVEL method  (STORET No. 00340), EPA
LOW LEVEL method (STORET No. 00335), and the AquaRator method.
The criteria considered in deciding which method to use for COD
determination were time necessary to obtain results, accuracy, and
acceptability of results.  Both EPA methods are well established
hut are time consuming.  The AquaRator, on the other hand is
extremely new and yields results in minutes.  A series of tests
Were run using two types of standard solutions to determine the
accuracy of each of these methods.  The results are given in-
Table 6.
The high level method was selected because it is widely accepted
and because it covers the required range of COD's.  It has a
""ajor drawback, however, because it takes about four hours to
obtain results.  The low level method was not used because of its
limited range, and because it was not felt to have any superior
a^curacy when compared to the other methods in the 30 to 50 ppm
COD range.
The usefulness of the AquaRator was the subject of continuous
discussion.   Results could be obtained in about 20 minutes.   At
tines the device would yield reproducible and fairly accurate
                                   63

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                           Table 6.  ACCURACY OF COD TESTING PROCEDURES
                                              mg/1
    STANDARD SOLUTION
    RUN NUMBER
                                 EPA HIGH LEVEL
                                   COD METHOD
                                STORET NO. 00340
SUCROSE
SODIUM ACETATE
                                       EPA LOW LEVEL
                                         COD METHOD
                                     STORET NO. 00335
SUCROSE
SODIUM ACETATE
 AQUARATOR
COD METHOD
  SUCROSE*
ON
•P-
COD
STANDARDS
mg/liter
10
30
50
120
250
500


15
32
52
124
266
551


14
28
48
125
267
549


14
32
54
123
261
551


10
26
44
106
240
484


12
26
44
107
230
478


12
21
52
108
227
476


18 12 14 11 9 8 13
35 36 32 31 31 32 29
55 57 57 46 46 46 45
116
221
423


12
30
44
117
215
428


12
31
46
118
223
423
     *  For AquaRator, sodium acetate solutions were used as standards.

-------
 results,  while at other times it  yielded  erratic  results.   Due to
 these  problems,  it was  not felt that  the  AquaRator  could be used
 for  determining  effluent COD's despite  the  speed  of obtaining  re-
 sults.  The AquaRator was used during the second  rainy  period  to
 aid  in determining recycle rate.   Because of  the  need to keep  net
 feed level  at  about  250 pptn COD,  up to  date results were required.
 The  EPA method was too  time consuming to  be used  as a control  aid.
 Another subject  of concern was the identification of COD materials,
 COD  is  referred  to in this report  as  if it  were a known, identi-
 fiable  substance,  but actually it  is  a wide variety of materials
 which can consume dissolved  oxygen.   These  materials can vary  in
 size from several atoms to large complicated molecules and  can be
 organic or  inorganic.   When these  various materials are adsorbed
 onto activated carbon they will all affect  the loading of the  car-
 bon  in  different ways.   For  this reason,  it would be of value  to
 know what materials make up  the COD in the  feed and effluent
 streams.  With a  knowledge of what is adsorbed and  what is not
 adsorbed,  improvements  in operations might  be made.
 An attempt was made to  identify the COD materials,  but due to  the
 small amounts and difficulty of analyzing hydrocarbons and water
 mixtures,  very limited  results were obtained.   These results were
 obtained by the United  States Environmental Protection Agency's
 Petroleum-Organic Chemicals Wastes Section, Treatment and Control
 Technology Branch and are given in Appendix C.  These findings
 indicated  the organic compounds in the effluent have a higher per-
 centage of higher molecular weight compounds than the feed.
More work  is needed in  the area before a true understanding COD
adsorption onto activated carbon can be attained.
                                  65

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REGENERATED CARBON TEST METHODS
A major effort was put forth during the two-year project to find a
reliable means to determine the quality of regenerated carbon.  The
major reason for the study was to give operating personnel a target
for furnace operation.
Two tests which were run on a regular basis during regenerations
are the apparent bulk density (ABD) test and the relative efficiency
(RE) test.  These test methods are described in detail in Appendix
B.  The apparent bulk density test takes about two minutes to run
and is simply a quick determination of unpacked density of the car-
bon.  The relative efficiency test is a time consuming comparison
of the adsorptive capacity of carbon sample with virgin carbon.
The criteria considered in selecting which test method to use as
an operational tool for the regenerator furnace were time required,
accuracy, and reliability of results.  During regenerations, operat-
ing personnel have relied on the ABD test simply because it can be
run on site in a couple of minutes.  If the delta ABD between
spent and regenerated carbon changes significantly from 0.06 gr/cc,
the operating personnel alter the burning rate.  The RE tests take
several hours to run and are, therefore, not used as an operational
tool.  The RE tests do, however, allow a more direct comparison of
adsorptive ability compared to virgin carbon.  The mode of opera-
tion used has resulted in carbon of essentially constant quality
based on RE tests within the limits of the determinations  Repre-
sentative ABD, Delta ABD, and RE data are given in Table 7.
Since, as described previously in this section, there are many
types of COD material with different adsorption characteristics,
it was decided to use process water instead of sucrose as a stan-
dard for the RE test.  This was done in the hope that the process
water would be more likely to be adsorbed in a similar matter as

                                  66

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           Table 7.  COMPARISON OF ABD AND RE TESTS

First Rains
Date
11/3/71
11-5-71
11-6-71
11-7-71
11-9-71
11-10-71
Second Rains
3-3-73
3-9-73
3-10-73
3-13-73
3-15-73
3-17-73
3-24-73
Regenerations
Regenerated Delta
ABD ABD
0.531
0.504 0.07
0.587
0.499
0.499
0.493
Regenerations*
^*
0.50 0.05
0.49 0.06
0.50 0.06
0.49 0.07
0.50 0.07
0.47 0.07
0.48 0.05
Relative
Efficiency
66%
59%
69%
72%
83%
82%
102
102
102
101
98
98
98
*Further data is given in Table 8 for the second rains regeneration.



                               67

-------
the carbon plant feed.  The results of the RE tests using the two
standards are compared in Table 8.  The RE tests using processs
water give erratic results.  This is believed to be due to the
fact that the process water used for the tests is obtained on
different days and thus is not a good standard.

Therefore, even though the sucrose RE test is not necessarily
representative of how COD material will adsorb, it appears to be
a better test for comparing regenerated carbons.
                                   68

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                           TABLE  3
      COMPARISON OF  RELATIVE  EFFICIENCY  TESTS
                   OR REGENERATED CARBON
   DATE
 1-19-73
 1-20-73
 1-21-73
 1-22-73
 1-23-73
 1-24-73
 1-26-73
 1-27-73
 1-28-73
 1-29-73
 1-30-73
 1-31-73
 2-1-73
 2-2-73
 2-3-73
 2-4-73
 2-5-73
 2-21-73
 2-22-73
 2-23-73
 2-24-73
 2-25-73"
 2-28-73
 3-1-73
 3-3-73
 3-4-73
 3-5-73
 3-6-73
 3-9-73
 3-10-73
 3-11-73
 3-12-73
 3-13-73
 3-14-73
 3-15-73
 3-16-73
 3-17-73
 3-18-73
 3-19-73
 3-20-73
3-21-73
3-23-73
3-24-73
3-25-73
 ABD _

 0.44
 0.41
 0.44
 0.44
 0.43
 0.43
 0.47
 0.48
 0.47
 0.45
 0.43
 0.45
 0.47
 0.48
 0.48
 0.46
 0.45
 0.46
 0.50
 0.50
 0.47
 0.44
 0.48
 0.52
 0.50
 0.52
 0.46
 0.45
 0.49
 0.50
 0.47
 0.48
 0.49
 0.48
 0.50
 0.48
 0.47
 0.46
 0.47
0.50
 0.48
0.50
0.48
0.46
  RE
 USING
SUCROSE

   98
   99
   98
  100
  100
  100
   99
  100
   98
   97
   99
   96
   99
   99
   99
   99
   99
  102
  102
  102
  102
  102
  102
   99
  102
  101
  101
  100
  102
  102
  102
  102
  101
  97
  98
  98
  98
  98
  99
  97
  98
  99
  98
  99
  RE
 USING
PROCESS
 WATER

  101
  103
  114
  101
  101
   98
   99
  100
   99
   96
   98
  101
  113
  111
  114
  114
  111
  116
  116
  120
  116
  118
  114
  113
  111
  111
  111
  110
  115
  116
  118
  118
  113
  105
  113
  113
  109
  109
  108
  108
  108
  108
  110
  111
                             69

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                                SECTION X
      QUANTITIES AND COSTS BASED ON CONDITIONS DURING THE PROJECT
During the two-year project, 172,040,000 gallons of water was pro-
cessed to load 1,643,700 pounds of carbon with 407,890 pounds of
COD.  This resulted in an average carbon loading of 0.25 pounds of
COD per pound of carbon.  The carbon was used as the rate of 9.5
pounds per 1000 gallons of water treated.  The average feed COD
was 249 ppm and the average effluent was 50 ppm.  Averaged data
for each of the three periods of operation is given in Table 9.
The data in Table 9 shows that the second rains single stage operation
had a slightly higher loading than the first rains single stage
operation, and a lower effluent COD.
The overall average cost to operate the plant was 49C per 1000 gal-
lons of water treated, or 24C per pound of COD removed from the
water.  The cost summaries are given for both years' operation in
Table 10.
As can be seen in Figure 10, the cost was greatly reduced the sec-
ond year of operation due to improvements in the system.  The
operating labor and carbon costs remained close to the same while
the repair labor and utilities costs accounted for the major de-
crease.
With the improved operation of the second year, the plant demon-
strated the ability to operate at only 40? per 1000 gallons of water
treated, or 18
-------
Table 9.  ADSORPTION DATA
FIRST RAINS - SINGLE STAGE
TWO STAGE TEST RUN
SECOND RAINS - SINGLE STAGE
TOTAL
FEED COD, ppm
AVERAGE HIGH
377 490*
235 395
233 345
249 490*
EFFLUENT
AVERAGE
67
47
48
50
COD, ppm
HIGH
158
105
95
158
CARBON LOADING
Ib. COD/lb. carbon
AVERAGE
0.23
0.22
0.26
0.25
HIGH
0.30
0.39
0.39
0.39
       *The high value of  490 ppm  COD  is based on  the assumption
        that  the peak of 900 ppm COD during run  5  of the first
        rains is invalid.

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           COST
                                    First Year
                                        Ctnts Per      Cans ?«r
                                     Thousand Gallons  !.b,  of COD
                                 S    Of Patar 'freatad
                         TABLE 10


                         COST  DATA


                             Second Year

                                 Cat-.ts Per     Cents Per
                               Thovsmcl Calicos  lb. of CCS
                          S    Of V'ifrpr Treated   Ueraovad
                                           Total

                                 Cents ?er      Cents Per
                              Thousand Gallons  Lh. of COD
                          S   Of tfetar Trs-aMd
           UTILITIES
                               12209
17
                                                                     8858
                                                                                                         21067
                                                                                                                      12
           RE?AIU
                                7553
11
                                                                     2699
                                                                                                         1C 251
           OPJSMIHG
                                847Q
11
                                                                                                         23-i/O
-J
KS
           CAJfflOH
                               10247
15
                        11532
11
                                                             21779
                                     13
                                5113
                                                                     2ns
                                                               7249
           TOTAt
                                                                    40197
                                                                                 40
                                                                                                         83789
           *X£SCELLABZCGS lUCL

                1,  Maiotenanc« overhead
                2.  Transportation



                3.  Ktlatenance coats  other than Labor

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                              SECTION XI
                              APPENDICES

Appendix
   A.   Test Methods Used for Analysis of Water
         High Level COD                                       74
         Low Level COD                                        76
         AquaRator COD                                        77
         Suspended Solids and Volatile Solids                 80
         Total Oil                                            81
         Turbidity                                            81
         Color                                                81
         Odor                                                 81
         Miscellaneous Test  Results                            81
         Table 1.   Lab Water for Adsorption  Plant              82,83
         During Second Rains
   B.   Test  Methods Used for Analysis of  Carbon               84
         Relative  Efficiency                                  84
         Apparent  Bulk Density                                 85
         Figure 1.  Apparent Density Vibrator Feed             86
         Figure 2.  Conditions - Glass or Metal                87
         Figure 3.  Metal Vibrator 26 Gauge Galvantized        88
         Sheet Metal
  C.   Determination of COD Materials                         89
        EPA  Internal Report                                   89

                                 73

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                            APPENDIX A

              TEST METHODS USED FOR ANALYSIS OF WATER

HIGH LEVEL COD
The method given below is a brief summary of EPA STORET No. 00340
taken from Methods for Chemical Analysis of Water and Wastes 1971,
Environmental Protection Agency Water Quality Office, Analytical
Quality Control Laboratory, Cincinnati, Ohio.  p.17.
                        HIGH LEVEL WET COD
                        (50 mg/1 & higher)
          APPARATUS
          500 ml flat bottom boiling flasks  24/40
          Condensers - 300 mm Liebig or equivalent
          Hot plates - 9 watts/in2

          REAGENTS
          0.25 N K2Cr2C7 (Containing 120 mg Sulfamic acid/liter
                          to eliminate nitrite N interference up
                          to 6 mg/1 N in a 20 ml sample)
          Cone. H2S04 + 22 mg AgS04/9# bottle
          0.10 N Fe(NH4)2(S04)2'6H20 (40 gm FAS + 20 ml cone H2S04
                                      diluted to 1 liter)
          Ferroin Indicator
          PROCEDURE
          1.  Place approximately 0.4 gm HgS04 and a few glass

                                    74

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     beads in a 500 ml boiling flask.

 2.   Add 20 ml of sample of aliquot +  H20.

 3.   Pipette 10 ml 0,25 N K2Cr20y  into the  boiling
     flask and connect it to the water cooled condenser,

 4.   Slowly pour 30 mis 1^04 + AG2S04 down the  top  of
     the condenser while swirling  the  boiling flask.
     (CAUTION wear safety glasses  and  rubber gloves)
     Reflux for 2 hours (or less if sufficient).

 5.   Cool and wash condenser down  with distilled water
     (90 mis).

 6.   Remove flask from condenser and cool to ambient
     temperature.   Add 2-3 drops Ferroin indicator.

 7.   Titrate  to Organge-Brown color with 0.10 N FAS
     which has  been recently standardized.

 8.   Run blank  with 20  mis  distilled water  and all
     reagents.

               COD  mg/1 -'  (A-B)C  x 8000
                           mis  sample

     Where  A = mis  0.10 N  FAS for blank
           B = mis  0.10 N  FAS for  sample
           C - Normality of FAS
STANDARDIZATION OF FAS

1.  Pipette 10 mis K2Cr207 into a 500 ml boiling flask
    and dilute to 100 mis.

2.  Add 30 mis cone. H2S04 without Ag2S04.  Cool and
    titrate with FAS.

                Normality FAS  =  2.5
                                 mis FAS
                        75

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LOW LEVEL COD
The method given below is a brief summary of EPA STORE! No. 00335,
taken from Methods for Chemical Analysis of Water and Wastes 1971
Environmental Protection Agency Water Quality Office, Analytical
Quality Control Laboratory, Cincinnati, Ohio, p. 19.
                         LOW LEVEL WET COD
                        (5 mg/1 to 50 mg/1)
          APPARATUS
          500 ml flat bottom boiling flasks 24/40
          Condensers - 300 mm Liebig or equivalent
          Hot plates - 9 watts/in2

          REAGENTS
          0.025 N K2Cr20y
          Cone. H2S04 + 23.5 gm AgS04/9# bottle
          HgS04
          Ferroin Indicator

          PROCEDURE
          1.  Place 1 gm HgS04 + 5.0 ml cone,
              H2S04 ancj a few glass beads in a
              500 ml boiling flask.
          2.  Place in ice bath and add 25 ml of
              0.025 N K2Cr207 and 70 ml
              Cone. H2S04 (with AgS04).
          3.  Add 50 ml of sample or aliquot + H20.
          4,  Apply heat to flask and reflux for two hours.
                                 76

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            5.   Cool and wash condenser down with distilled
                water (25 ml).
            6.   Remove flask from condenser  and  cool  to  ambient
                temperature.  Add 8  to  10  drops  of Ferroin  indicator.
            7.   Titrate  to reddish hue  with  0.025  Fe(NH4)2(S04)2
                6H20
            8.   Run blank with 50 ml of distilled  water  and all
                reagents.
                         COD mg/1  =   (A-B) C x 8000
                                            S
               Where  A = mis 0.025 N Fe(NH4)2(S04)2 for blank
                      B = mis 0.025 N Fe(NH4)2(S04)2 for sample
                      C = Normality of Fe(NH4)2(S04')2
                      S = mis of sample
AQUARATOR COD
The  theory of  the AquaRator  is  given below.  The operation of  the
instrument is  not given  in this report, but  is given in "LIRA
INFRARED Analysed Model  300, Theory - Operation and Service Manual"
Mine Safety Appliances Company,  201 North Braddock Avenue, Pitts-
burg, Pennsylvania.
.Theory of Operation
     Quoted from "Lira Infrared Analyser Model 300, Theory -
     Operation and Service Manual" Mine Safety Appliance
     Company, 201 North Braddock Avenue, Fittsburg, Pennsyl-
     vania,  pp. 10,  11.
     The LIRA is based on the principle of infrared absorp-
     tion.   It is a common physical fact that all molecules,
     with the exception of elemental gases,  exhibit character-
     istic absorption spectra that is  related to  the number

                                   77

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configuration, and type of atmos in this molecule.
The more simple the molecular structure, the simpler
the absorption spectrum and conversely, heavy com-
plicated molecules exhibit quite complex spectra
By examination of the infrared spectra of the com-
ponents in a process stream, it is normally possible
to locate an infrared absorption band unique to the
"component of interest."  The LIRA detector gas,
filter gas, interrupter and window materials are
selected so that the optics are sensitized ("tuned")
only to this unique absorption band of the "component
of interest."  The cell length is determined by the
intensity of the absorption band and the calibration
range of the instrument.  LIRA optics and sensitiza-
tions are in good agreement with the "Lambert-Beer"
law of light absorption.
In general, the LIRA sources direct two identical
infrared beams through two parallel, gold plated,
polished stainless steel gas cells housed in a solid
aluminum block.  One cell contains a known comparison
gas, the other the sample (unknown) gas.  After the
radiation beams pass through the gas cells they are
directed into a single detector unit that contains
a sealed-in gas.  As the gas in the detector absorbs
infrared radiation, there is a temperature and result-
ing pressure increase of the detector gas.  The in-
creased pressure moves a sensitive membrane in the
detector unit.  The movement results in a capaci-
tance change in the detector and this capacitance
change is converted to an output signal by the
electronic amplifier.
                             78

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 Between the infrared sources and the gas cells, a
 half-circle interrupter element or beanj-^chopper
 rotates at two cycles per second.  As it rotates,
 It alternately blocks the infrared radiation beam
 from each source, permitting only one beam at a time
 to pass through the gas cells and enter the detector
 unit.   The detector thus alternately responds to the
 infrared adsorption of the gases in each cell.   As
 long as the energy at the detector is equal in both
 beams,  a properly aligned instrument will read  zero.
 When the gas  to be analyzed (the "component of  interest")
 is introduced into the sample cell,  it  absorbs  some of
 the detectable infrared energy and thus reduced the beam
 radiation that reaches  the detector  unit from the
 sample  cell.   As  a result,  the two beams become unequal
 and the radiation entering the detector flickers  as
 the beams  are  alternated.   (The brighter comparison
 gas beam,  then the dimmer  sample gas  beam,  etc.)
 The detector gas  expands and  contracts with this
 flicker and directly  indicates  the energy difference
 between the two beams.  This variation generates  an
 electrical signal which is proportional  to  the  infra-
 red  energy difference between  the  two beams.
 The  electronic circuit is tuned  so that  only variations
 between the intensity of the beams entering the detector
 unit produce an output signal.  When the beams are un-
 equal the instrument produces an output  signal that can
be measured.  The output signal is quickly read (90%
of final reading within 5 seconds) on the meter or tran-
scribed on an auxiliary recorder.
                              79

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     Selectivity to the "component of interest" is obtained
     by (a) the detector gas, (b) window and interrupter
     materials, and (c) filter gases.  These sensitizing
     components and sample cell lengths vary with the
     application.  Most LIRA Model 300 Analyzers will
     operate on gains 2, 3, or 4, but some special high
     sensitivity applications will perform adequately
     on gain position 5.
SUSPENDED SOLIDS AND VOLATILE SOLIDS
The method given below is a brief summary of the Suspended Solids
and Volatile Solids test given in Standard Methods for the
Examination of Water and Wastewater. 13th Edition, P 538, Method
224D (1971).  The equipment and furnace temperature are altered
slightly from the cited method.
     Equipment:  Milipore Filter Apparatus
                 Crucibles
                 Glass Fiber Filters - Reeve Angel 4.25 cm
                 Grade 934 AH
     Procedure:  1.
Dry crucible and glass filter in 103°C
oven and place in dessicator to cool.
Obtain tare weight (A).
                 2.   Place glass filter on Millipore filter
                     apparatus and vacuum 20-50 mis of sample
                     through filter.
                 3.   Rinse any adhering material from sides
                     of Millipore filter apparatus with dis-
                     tilled water.
                 4.
Dry glass filter in a 103°C oven for
2 hours.
                 5.   Cool in a dessicator and weigh (B).
                             SUSPENDED SOLIDS ppm - (B-A)  x 10
                 6.
                               mis sample
Place crucible and filter in 600°C
(1112°F) Furnace for 10 minutes.
                                   80

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                   7.  Cool in a dessicator and reweigh (C).
                                                        CB-C
                                                        mis sample
VOLATILE SUSPENDED SOLIDS - CB-C x IQ6)
 TOTAL OIL
 The total oil was determined by APRA Standards,  Part 137:
 Petroleum Ether Extraction,  13th Ed., pp 254-257.
 TURBIDITY
 The turbidity was determined using  a Each Turbidimeter using
 Jackson turbidity units.
 COLOR
 The color was measured by ASTM D-1209 using cobalt-platinum color
 standard.
 ODOR
 The  odor was measured by APHA, Part 136:  Odor.
MISCELLANEOUS  TEST RESULTS
The total oil and Suspended Solids test were run on a regular
basis along with the pH.  The laboratory data from January 1973
is given in Table 1.  This data is typical of that obtained
throughout the project.
                                 81

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                       APPENDIX A
Table 1.  LAB DATA FOR ADSORPTION PLANT DURING SECOND RAINS

DATE
1-18-73
1-19-73
1-20-73
1-21-73
1-22-73
1-23-73
1-24-73
1-25-73
1-26-73
1-27-73
1-28-73
1-29-73
STREAM
FEED
EFFLUENT
FEED
EFFLUENT
FEED
EFFLUENT
FEED
EFFLUENT
FEED
EFFLUENT
FEED
EFFLUENT
FEED
EFFLUENT
FEED
EFFLUENT
FEED
EFFLUENT
FEED
EFFLUENT
FEED
EFFLUENT
FEED
EFFLUENT
PH
7.2
6.9
7.2
7.1
7.0
6.8
7.0
7.2
7.1
7.1
6.9
6.6
6.8
6.7
7.4
7.3
6.8
6.8
7.1
6.9
6.8
6.8
6.8
6.8
COD
320
95
245
25
265
25
335
20
335
20
345
50
295
40
270
50
260
45
250
70
240
55
220
55
TOTAL
OIL

34
1
27
9
29
13
18
11
23
6
20
17
26
6
29
7
32
16
22
8
19
7
SUSPENDED
OIL
29
12
16
10
24
12
35
17
17
14
27
17
14
9
16
8
16
11
51
15
15
2
14
3
                            82

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Table 1 (cont'd).  LAB DATA FOR ADSORPTION PLANT DURING SECOND RAINS
                                             TOTAL      SUSPENDED
     DATE        STREAM       PH      COD       OIL         OIL

    1-30-73     FEED            7.1      205       32          20
               EFFLUENT       7.1       50       16           6

    1-31-73     FEED            7.0      175       53          23
               EFFLUENT       7.1       40       41           4
                                     83

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                            APPENDIX B


             TEST METHOD USED FOR ANALYSIS OF CARBON


RELATIVE EFFICIENCY

The method given below is the relative efficiency test developed

by Atlantic Richfield Company.
                     RELATIVE EFFICIENCY TEST
                       FOR ACTIVATED CARBON
          1.  About five grams of each carbon sample to be
              analyzed is oven-dried for three hours at 110°C.

          2.  Upon cooling to room temperature, each sample
              is individually ground to yield a few grams  of
              +325 mesh powder.

          3.  One gram (± 0.01 gm) portions of each sample is
              mixed with a 50 ml aliquot of standard solution
              (COD concentration = A ppm) in 125 ml Erlenmeyer
              flasks.  The flasks are well stoppered and shaken
              for one hour on a laboratory shaker.

          4.  After shaking,  the COD of the aqueous phase  is
              measured (B ppm).

          5.  The 100% efficiency reference is provided by treat-
              ing a virgin sample of activated carbon according
              to steps 1 through 4.

          6.  The relative efficiency is calculated as

                 Relative Efficiency, %   (A-B)
                                        m   A   Sample
                                          TOT"
                                            A   Reference
                                  84

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APPARENT BULK DENSITY

The method given below is the Apparent Bulk Density test used

during the project.


                       APPARENT DENSITY TEST


          EQUIPMENT REQUIRED

          1.   Vibrator Feeder - See Figures 1 through 3.

          2.   Cylinder, graduated,  capacity 100 ml.

          3.   Balance having a sensitivity of 0.1 g.


          PROCEDURE

          1.   100 ml.  of the carbon is dried to constant
              weight at 150  ± 5°C or taken dry from  furnace
              discharge chute.

          2.   Sample is placed  into the reservoir funnel so
              that the material does not prematurely  flow into
              the graduated  cylinder.

          3.   yhe sample is  added to the cylinder from the
              vibrator feeder through the feed funnel.

          4.   Fill the cylinder at  a uniform rate of  0.75  to
              1.0 ml.  per second, up to the  100 ml mark.   The
              rate can be adjusted  by  changing the slope of the
             metal  vibrator  and/or by raising or lowering the
              reservoir funnel.

         5.  Transfer  the contents  from  the  cylinder to a
             balance pan and weigh  to  the nearest tenth of a
             gram (O.lg).


          CALCULATIONS

          Calculate the apparent density as follows:

          Apparent Density,  g/ml «=  weight of activated carbon-pn
                                              100

                                 85

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                                                        RESERVOIR FUNNEL
                                                        CLAMPED TO RING STAND
                                                        RING STAND
                                                        METAL VIBRATOR
                                                        DOOR BELL "BUZZER"
                                                        (FOR 10 VOLT SERVICE)
                                                             60 CYCLE



—
—
^.


/
7











FEED FUNNE
TO RING SI
inn-mi. A5
CYLINDER
/ 	 	 rUTTPH
(SPST BA1
-rfr /
h1 //
PI //
                                                                   TRANSFORMER
                                                                   (PRI. VOLTS
                                                                       VA
                                                                   SCC. VOLTS  6-
                                                                   CYCLES      50-ou
                                                                                    ,
                                                                                   '
Appendix B, Figure 1.  Apparent Density Vibrator Feeder

                                 86

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00
                                                                                             •y i /o" .. .	
                                                                                             O I / C.        " -•••••—'- —™..™-— «.——	
                                                                                           p-15/16  ~
                            Appendix  B,  Figure 2.  Conditions:  -  Glass  or Metal

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00
00
                       Appendix Bf  Figure  3.  Metal Vibrator - 26 Gauge Galvanized Sheet Metal

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                              APPENDIX C
                    DETERMINATION OF COD MATERIALS
On April 17, 1973, the United States Environmental Protection
Agency in a report to Mr. Leon H. Myers, Chief, Petroleum-
Organic Chemicals Wastes Section, Treatment and Control Technology
Branch; from Mr. Billy L. DePrater, Supervisory Research Chemist,
Petroleum-Organic Chemicals Wastes Section, Treatment and Control
Technology Branch, gave the results of numerous tests on various
Watson Carbon Plant streams.  These tests included an attempt at
a determination of the types of COD involved in the feed and
effluent.   The report is given below.
The numerous gas chromatographs referred to are not given in this
report, and interested readers are referred to the original report.
                          EPA INTERNAL REPORT
                       ORGANICS IN ARCO SAMPLES
     The drganics were extracted from the Arco samples for
     analyses by gas chromatography to obtain a "finger-
     print" of the organics present and also to measure the
     amount of organics as determined by the area under the
     chromatograms.
     The procedure for extraction of the water samples was
     to measure 500 ml of sample (750 ml in the case of
     "Eff  New Cell")  into a two liter separatory funnel and
     add 20 ml of redistilled chloroform.   After shaking
     about two minutes the phases were allowed to separate,
     and the chloroform phase was drained  into a small
     column of sodium sulfate which had been washed with
                                  89

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 chloroform.  The sodium sulfate column removed water
 and broke any emulsion that was present.  Two more
 extractions were made on the sample using 15 ml of chloro-
 form each time, so that the total volume of chloroform
 used was 50 ml.
 After extracting the water samples, the extracts were
 concentrated by evaporating the chloroform with a
 gentle stream of air until the solutions were con-
 centrated enough to run gas chromatographic analyses.
 The two effluent extracts contained a very small amount
 of organics, so the chloroform was evaporated until the
 volume of each was 0.1 ml.  The other extracts were
 sufficiently concentrated after evaporation of the
 chloroform to a remaining volume of 1 ml.
 Samples of spent carbon and regenerated carbon were
 extracted in a Soxhlet extraction apparatus.  The
 spent carbon first was placed in a shallow pan on a
 steam bath to evaporate the water.  After two hours
 the spent carbon appeared to be dry so samples of about
 100 ml of each carbon was weighed and put into the
 extractors with glass wool at the bottom to prevent
 carbon particles from getting into the siphon tubes.
 Each flask contained 300 ml of chloroform and steam
 was used to heat the flasks and maintain a cycling
 rate of four times per hour for 24 hours.  The extracts
 were then distilled to reduce the volume from 300 down
 to 50 ml before analysis by gas chromatography.
 Gas chromatographic analyses were run with a 6* x 1/8"
 stainless steel, Dexsil 300 column.  The temperature
 was programmed from 50 to 350°C at eight degrees per
minute, and an electronic integrator was used to
                            90

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 measure the total area under  the chromatogram for  quan-^
 titation of the sample.  Solvent oil mixtures were used
 for calibration by running mixtures containing 0.06,
 0.12,  and 0.24 mg of  oil.  The  area measurements obtained
 were plotted versus the milligrams of  sample.   A mixture
 of  n-paraffins was run under  identical conditions  to
 indicate the boiling  range of the samples by  the chromato-
 grams.   Data from the area of the chromatogram, volume
 of  water extracted (or grams  of  carbon extracted), volume
 of  concentrated extract, and  volume charged to the gas
 chromatograph gave the following information:
            Eff.  New Cell             0.63 mg  oil/liter
            Carbon Plant Total Eff.   1.73 "     "  "
            Carbon Plant Total Feed  34.8  "     "  "
            Carbon Plant Total Feed  34.3  "     "  "
            Res  505                111    "     "  "
            Feed to Res  505          68.8  "     "  "
            Spent  Carbon            19    mg oil/gm.
            Regenerated  Carbon       0    "     "  "
 Copies of  the chromatograms are attached.  The  total
 area between  four minutes: and 42 minutes was measured
 using the baseline set  at the beginning of the run.
 Corrections were made for area due to the solvent tail
 and drift due to stationary phase bleed that occurs
 toward the end of  the run.
 The following observations are made by comparison of
 Eff. New Cell and  Carbon Plant Total Eff. chromatograms.
 It is obvious that the carbon plant total effluent
 contains a greater amount of organics since the chromato-
 graph is higher above the baseline throughout most of the
run.  The prominent peak at 28 minutes retention time
is very likely a phthalate compound used as a plasti-
cizer in the liner of  the screw.cap on the container.
                             91

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The caps, were supposed to have Teflon liners, but
appeared to be only a Teflon coating which apparently
was not impervious to the chloroform solvent.  The
carbon was less efficient for removing the organic
compounds represented by peaks at 12 and 12.4 minutes
retention time.
The composition of the organics remaining after carbon
treatment consists of a higher percentage of high boiling
compounds when compared to the organics in the feed.
This is illustrated by plotting corrected area percent-
ages of the total area between four and 42 minutes
retention time on the chromatograms for carbon plant
total effluent and carbon plant total feed.  The
plots show that 70 percent of the organics in the feed
have a retention time of less than 22 minutes or boil
below 657°F.  The 70 percent point of the effluent is
at about 28.8 minutes retention time or about 789°F.
If a visual comparison of peaks and areas is made, it
must be remembered that the effluent sample-solvent
volume was 0.1 ml while the feed sample-solvent volume
was 1 ml.  There is a factor of two difference in
attenuation on the feed and effluent chromatograms
or a total magnification of 20 on the effluent chromato-
gram.  Several normal paraffin retention times obtained
from the temperature calibration runs are shown on the
feed and effluent chromatograms, and it is noted that
they correspond closely to some of the sample peaks.
All of the chromatograms may be compared on the basis
of peak retention times and approximate boiling points
and boiling ranges; but as noted before, visual area
comparisons and peak height comparisons must take into
consideration the attenuation and concentration of the
sample.
                             92

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                              TECHNICAL REPORT DATA
                        (Please read Instructions on the reverse before completing)
1. REPORT NO.
  EPA-660/2-75-020
                                                  3, RECIPIENT'S ACCESSIOC+NO.
4. TITLE AND SUBTITLE
 Refinery Effluent  Water Treatment  Plant Using
 Activated Carbon
           5. REPORT DATE
             "   1975
May
           6. PERFORMING ORGANIZATION CODE
7. AUTHOR(S)
 Gary C. Loop
                                                  8. PERFORMING ORGANIZATION REPORT NO,
9. PERFORMING ORGANIZATION NAME AND ADDRESS
 Atlantic Richfield  Company
 Carson, California
            10. PROGRAM ELEMENT NO.
              1BB036
            11. CONTRACT/GRANT NO.
                                                     12050 GTR
12, SPONSORING AGENCY NAME AND ADDRESS
            13. TYPE OF REPORT AND PERIOD COVERED
U.S.  Environmental  Protection Agency
Robert S. Kerr Environmental Research Laboratoify*
P.O.  Box 1198
Ada,  Oklahoma 74820
             Demo  1971^1974
             . SPONSORING AGENCY CODE
IB. SUPPLEMENTARY NOTES
Prepared in cooperation with the  Petroleum/Organic  Chemicals Wastes
Section, Robert S.  Kerr Environmental  Research Laboratory, Ada, Okla,748
16. ABSTRACT
Reduction of Chemical  Oxygen Demand  (COD) in petroleum refinery effluent
wastewater by adsorption onto activated carbon was  demonstrated on  a
commercial level during a two-year project at Carson,  California.   The
plant  contained over  750,000 pounds  of carbon, regenerated 1,644,000
pounds of carbon,'processed 172 million gallons of  water, and removed
408,000 pounds of COD.
The  carbon was exhausted at the rate of 9.5 pounds  per 1000 gallons of
water  processed.  At  an average feed COD concentration of 250 ppm and an
average effluent COD  concentration of 50 ppm, the carbon was loaded to
an average of 0.26 pounds of COD per pound of carbon.   Following  solutioi
of initial startup problems, the unit was operated  at  a cost of 40  cents
per  1000 gallons of water treated, or 18 cents per  pound of COD removed.
7.
                           KEY WORDS AND DOCUMENT ANALYSIS
               DESCRIPTORS
b.lDENTIFIERS/OPEN ENDED TERMS  C. COSATI Field/Group
Activated carbon, Adsorption, Organi
loading,  Oxygen demand,  Pollution
abatement,  Settling basins,  Waste*
water  treatment, Carbon  regeneration
Chemical  oxygen demand
   Intermittent  carboi
  treatment plant,  Ca.'.
  gon process, Rainfa]
  runoff
8. DISTRIBUTION STATEMENT

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                       22. PRICE
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                       * U. S. GOVERNMENT PRINTING OFFICE: 1975-698.909 /4 REGION 10

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