EPA-600/2-76-294
December 1976
Environmental Protection Technology Series

            TREATMENT  OF  EFFLUENT  WATERS  FROM
                              VEGETABLE OIL REFINING

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                                 Industrial Environmental Research Laboratory
                                      Office of Research and Development
                                     U.S. Environmental Protection Agency
                                             Cincinnati, Ohio 45268

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                RESEARCH REPORTING SERIES

Research reports of the Office of Research and Development, U.S. Environmental
Protection Agency, have  been grouped  into five series. These five broad
categories were established to facilitate further development and application of
environmental technology. Elimination of traditional grouping was consciously
planned to foster technology transfer and a maximum interface in related fields.
The five series are:
     1.    Environmental Health Effects Research
     2.    Environmental Protection Technology
     3.    Ecological Research
     4.    Environmental Monitoring
     5.    Socioeconomic Environmental Studies

This report  has been  assigned to the ENVIRONMENTAL PROTECTION
TECHNOLOGY series. This series describes research performed to develop and
demonstrate  instrumentation, equipment, and methodology to repair or prevent
environmental degradation from point and non-point sources of pollution. This
work provides  the new or improved technology  required for the control and
treatment of pollution sources to meet environmental quality standards.
This document is available to the public through the National Technical Informa-
tion Service, Springfield, Virginia 22161.

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                                         EPA 600/2-76-294
                                         December 1976
        TREATMENT  OF EFFLUENT WATERS

         FROM VEGETABLE  OIL  REFINING



                     by
             Donald F.  Gill,  Jr.
               James C. lelase
         Archer Daniels Midland Co.
           Decatur, Illinois  62525
               Grant 12060 FDK
               Project Officer

            Clifford Risley, Jr.
    U.S. Environmental Protection Agency
                  Region V
           Chicago, Illinois 60606
INDUSTRIAL ENVIRONMENTAL RESEARCH LABORATORY
     OFFICE OF RESEARCH AND DEVELOPMENT
    U.S. ENVIRONMENTAL PROTECTION AGENCY
           CINCINNATI, OHIO 45268

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                                  DISCLAIMER


     This report has been reviewed by the Industrial  Environmental  Research
Laboratory, U.S. Environmental Protection Agency, and approved for  publication-
Approval does not signify that the contents necessarily reflect the views and
policies of the U.S. Environmental Protection Agency, nor does mention of
trade names or commercial products constitute endorsement or recommendation
for use.
                                      n

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                                FOREWORD


     When energy and material resources are extracted, processed, con-
verted, and used, the related pollutional impacts on our environment and
even on our health often require that new and increasingly more efficient
pollution control methods be used.  The Industrial Environmental Research
Laboratory - Cincinnati (lERL-Ci) assists in developing and demonstrating
new and improved methodologies that will meet these needs both efficiently
and economically.

     This report, entitled "Treatment of Effluent Waters from Vegetable
Oil Refining." presents the development of a chemical pretreatment method.
Waste management personnel can utilize the results to reduce the BOD load
up to 71%.  The Industrial Pollution Control Division and the project officer
can be contacted for further information on the subject.
                                    David G. Stephan
                                        Director
                       Industrial Environmental Research Laboratory
                                       Cincinnati
                                       iii

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                                ABSTRACT
     With overloaded municipal facilities and increasingly restrictive
Federal water quality regulations, it has become necessary to restrict
industrial wasteloads.  Vegetable oil refineries generate a high BOD5
loading along with a high fat loading, which makes treatment difficult.
Original loadings with only surface skimming as treatment generated 0.0135
kg BOD5 per kg oil processed.  After the grant period, the load was 0.0019
kg per kg processed for a reduction of 86%.

     Major wastewater sources and processes are defined and described.
Refinery washwater from the oil water wash centrifuges was found to be the
major contributor of BODs and fat, with barometric cooling tower blowdown
and water from acidulation contributing smaller amounts to the load.

     A calcium chloride pretreatment for the washwater which reduced the
overall BODs load by 71% was developed.  This was done by the addition of
0.25% by weight calcium chloride to the washwater and pH adjustment to
between 5 and 6.  Further research was done to devise methods to further
reduce the wastewater loadings to within municipal limits.  Dissolved air
flotation was tried without success.  A consultant was retained to inves-
tigate further chemical preatment.  These studies along with the recom-
mended process for ferric chloride and lime treatment are presented.

     It was felt by the grantee that the wastewater loads could be reduced
to within the municipal limits by making some process modifications, in-
creasing production supervision, and installing a clarifier to control
process upsets.  This program resulted in a further reduction of 50%
and brought the waste strength to within municipal limits.

     Cost for the system installed is $75,000 per year.  Revenues from
recovered by-products range from $20,000 per year to $180,000 per year,
depending on the price of recovered material.

     This report was submitted in fulfillment of Grant Number 12060 FDK
by the Archer Daniels Midland Company, Decatur, Illinois, under the partial
sponsorship of the U.S. Environmental Protection Agency.  This report
covers a period from March 1970 to December 1973.
                                       iv

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                                CONTENTS

Foreword	iii
Abstract	    iv
Figures	    vi
Tables	viii
Acknowledgment 	     x
Introduction 	     1
Conclusions  	     2
Reconraendations  	     4
Process Description   	     5
Wastewater Sources, Analysis, and Quantities  	    11
Primary Chemical Treatment  	   16
Treatability Studies  and  Design Basis   	   20
Description and Evaluation  of Installed Wastewater  ....   48
Management Facilities
Appendices	   68
Bibliography	   77

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                                 FIGURES

Number                                                          Page
  1     Soybean preparation and oil  extraction flow
        diagram (typical Lincoln & Decatur) 	    6
  2     Oil refining flow diagram   	    7
  3     Deodorization flow diagram  	   10
  4     BOD5 and COD correlation for total West plant
        effluent	12
  5     Schematic of majonwastewater sources	13
  6     CaClp water treatment flow sheet  	   19
  7     Treatment flow diagram during water survey  	   23
  8     West plant refinery skimmer effluent variability of
        24 hr composite COD and flows 	   33
  9     West plant refinery treated  skimmer effluent
        settling test results	37
 10     Proposed treatment facility 	   39
 11     Decatur wastewater treatment facility 	   49
 12     West plant treatment flow diagram 	   51
 13     Pounds BODg per pound oil processed	   52
 14     Pounds fat per pound oil processed	53
 15     Clarifier pH vs. day ADM Decatur	60
 16     Temperature vs. day ADM clarifier, Decatur,
        Illinois	61
 17     Clarifier COD vs. day ADM Decatur	62
 18     Fat vs. day Decatur ADM clarifier	63
                                     vi

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Number                                                         Page
 A-l    Rex wastewater clarifier	   68
 A-2    Walker skimmer	69
 C-l    Lincoln wastewater treatment facility  	   71
 C-2    ADM Lincoln, Nebraska average mg/1  fat vs.  month
        January 1971-March 1972  	   74
 C-3    ADM Lincoln, Nebraska suspended solids vs.  month
        January 1971-March 1972  	   75
 C-4    ADM Lincoln, Nebraska average Ib COD/day vs.  month
        January 1971-March 1972  	   76

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                                 TABLES
Number                                                         Page
  1     Characteristics of Refinery Wastewater
        Component Streams Grab Samples 	  14
  2     Extraction Plant Loading ....  	  15
  3     Laboratory Washwater COD Reduction by Calcium
        Chloride Treatment and pH Adjustment 	  16
  4     Wastewater BODs Before and After CaCl2 Treatment
        Installation:  East Plant Discharge to Municipal
        Sewer	17
  5     Laboratory COD Reduction with Gas Flotation  	  21
  6     Chemical Flocculation Screening Test Results for
        West Refinery Skimmer Effluent 	  24
  7     Chemical Flocculation Results of Samples of West
        Plant Refinery Skimmer Effluent  	  30
  8     Laboratory Settling Test Results  of Refinery
        Skimmer Effluent 	  34
  9     Summary of Investigative Results  	  35
 10     Summary of Design Basis and Major Unit Sizes 	  40
 11     Summary of Major Equipment Sizes  	  41
 12     Summary of Construction Costs  	  45
 13     Summary of Annual Estimated Costs  	  46
 14     West Plant Effluent Analysis 	  54
 15     Decatur West Plant BODs and Fat Per Pound
        Oil  Processed	56
 16     Clarifier COD Reduction	58
                                    viii

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Number                                                         Page
 17     Decatur Clarifier Operation 	    64
 18     Lagoon Operation COD (mg/1) 	    65
 19     Installation and Operation Costs for West .  .  .
        Refinery Waste Treatment System 	    66
 20     Summary of Treatment Costs	    66
 21     Net Costs .  .	    67
 C-l    Analysis of Discharge to Municipal Sewer  	    72
                                      IX

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                                ACKNOWLEDGMENTS


     This study was conducted by the Archer Daniels  Midland  Company,  Decatur,
Illinois.  The initial treatment studies were conducted by James  lelase  under
the direction of R. S. White.  In 1969,  James lelase took over direction of
the study.  The Roy F. Weston Company of Chicago,  Illinois,  was retained to
investigate secondary chemical  treatment and to  design a ferric chloride and
lime treatment system.  Arnold Johnson,  refinery project engineer,  supervised
construction of the clarifier and treatment system.   Donald  Gill  developed
the operation procedures and process modifications after the system was  in-
stalled and prepared the final  report.  James Curry  assisted with the analyt-
ical work throughout the grant period.

     This report was submitted in fulfillment of Grant No. 12060  FDK.  Clifford
Risley, Jr. was the project officer during the grant.  David Rickles  was the
assistant project officer during the research and construction phase.  Ronald
Eng was the assistant project officer during the preparation of the final
report.  He and James Scaief, research representative, Corvallis, Oregon,
provided assistance in the final report  preparation.  Special recognition
is made of the efforts of Jack L. Witherow of the Food and Wood Products
Branch, Corvallis Field Station, lERL-Cincinnati.  Mr. George Rey,  EPA staff
engineer, Washington Headquarters, provided technical assistance  in the  early
stages of the project.

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                                  SECTION I

                                INTRODUCTION
     The Archer Daniels Midland Co., Inc., processes oilseeds, primarily
soybeans.  Oil is solvent-extracted from the seeds and refined at three
locations—two at Decatur, Illinois, and one at Lincoln, Nebraska.   The
refining of vegetable oils generates several wastewater streams that have
caused the plants to exceed acceptable waste strength limits set by their
respective municipal authorities.  The object of this project was to
analyze these waste streams and devise treatment methods by which their
     and fat strength could be reduced to acceptable levels.
     The initial problem was to identify the waste streams and to charac-
terize the wastewater.  The second problem was to determine optimum treat-
ment for each source and finally to implement the necessary equipment and
procedures.

     The initial investigation and design was done by ADM in conjunction
with a consulting firm.  These investigations are described in Sections
V, VI, and VII.

     Because of significant process modifications described in Section
VIII, it was determined that some of the process recommendations would not
be necessary.  Provisions were made for their future installation if they
proved to be necessary.

     A description of equipment installed and results obtained are con-
tained in Section VIII.

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                                 SECTION II

                                 CONCLUSIONS
     The wastewater survey done after the calcium chloride system was
installed determined that for a soybean processing facility,  the refinery
produces approximately 90% of the wasteload and the extraction plant con-
tributes only about 10%.  Of the refinery wastewaters,  the washwater is
the largest source of BODs and fat.   For a facility processing 385,500 kg
(850,000 Ib) per day of oil, this stream contributes 450 to 22,700 kg
(1000 to 50,000 Ib) per day of BODs  and fat in the form of water soluble
soaps.  Greasy cooling water can contribute 340 kg (750 Ib) of fat and
BODs.  Acid water contributes approximately 30 kg (70 Ib) of fat and
1800 kg (4000 Ib) of BODs per day.  Floor washings and car washings can
contribute significant and highly variable loadings.  Any of these sources
can contribute many times the normal loading under conditions where the
process is upset or uncontrolled.

     Treatment of the washwater with 0.25% by weight calcium chloride
resulted in an overall reduction of  71% of the 8005, from 0.0135 to 0.0039
kg BODs per kg oil processed.  Process modifications, increased process
control, and a clarifier resulted in a further reduction in total load of
50% of both the fat and COD.  A greater reduction would have been obtained
had the plant not started to refine  corn oil at approximately the same time
the clarifier was started.  Installation of the clarifier in Lincoln, where
corn oil is not refined, resulted in a reduction of 65% of the COD and fat.
The overall reduction in Decatur for both the calcium chloride and clarifier
was 86%, from 0.0135 kg BODs per kg  oil processed to 0.0019 kg BODs per kg
oil processed.

     Laboratory studies indicated that secondary chemical treatment with
ferric chloride and lime would result in a reduction of 85% of the fat and
65% of the COD over the calcium chloride treatment.  This would be an overall
reduction of 95% of the fat and 90%  of the COD.

     The calcium chloride treatment  system was installed in 1970 at a cost
of $25,000.  Treatment cost based on 10 years straight line depreciation is
$32,308 per year.  The system removes approximately 1206 kg (2660 Ib)
per day fat and 3736 kg (8236 Ib) per day BODc.  This is a cost of 2.34$
per kg (1.06
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mately 778 kg {1716 lb) per day BODs and 190 kg  {420  Ib)  per day fat.
This is a cost of 61.954 per kg {28.U per lb) fat and  15.154 per kg
(6.874 per lb) BOD5 removed.

     The net cost for the treatment system is 14.774  per  kg  (6.7$ per lb)
fat removed, 4.564 per kg (2.074 per Ib) BODs removed,  and 364 per 1000
liter ($1.36 per 1000 gal) water treated.  This  cost  is offset by revenue
from recovered oil that can be sold.  The price  of this oil  has varied over
the grant period from 8.84 to 39.7* per kg (44 to 184 per lb).  This results
in a net treatment cost that has varied from 254 per  1000 liter  (954 per
1000 gal) to a gain of-514 per 1000 liter ($1.93 per  1000 gal).  On a
basis of oil processed, this is .0324 per kg (.0154 per lb)  oil processed
to a gain of .0634 per kg (.0284 per lb) oil processed.

     Installation of the ferric chloride and lime treatment  system is
estimated to cost $100,300 per year compared to  $43,000 for  the system
installed,  The estimated fat recovered would be approximately 324 kg
(714 lb) per day at a cost of $275 per day, or 84.94  per  kg  (38.54 per lb)
fat, which is 31% higher than the installed treatment.

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                                 SECTION III

                               RECOMMENDATIONS
     Further research should be done to develop uses for and modifications
of corn lecithin to reduce the wasteload from refining corn oil.

     Additional study is also needed to determine the effect the  ferric
chloride and lime treatment system would have on the reduced waste load
compared to the load at the time the secondary chemical treatment was done.

     A further major reduction in 6005 would result in the development of a
good treatment system for the acid liquor.  This was not an important consi-
deration during this grant period because after the development of the
calcium chloride treatment for wash water, the plant was well within the
BOD5 limit specified by the municipality.

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                                 SECTION IV

                             PROCESS DESCRIPTION


     This section describes a soybean extraction plant and refinery common
to Decatur and Lincoln.  Additional corn germ extraction and refining in
Decatur is entirely analagous to the soybean process and will not be
described separately.  Only those processes that generate significant
waste products will be described in detail.  All processes operate 24 hours
per day and 7 days per week.  The plant in Decatur has the capacity for
120,000 bushels per day soybean extraction, and 200 tons per day of corn
germ, and the capacity to refine 1.4 million Ib per day of vegetable oil.
Figures 1 and 2 describe extraction and oil refining respectively.

SOYBEAN PREPARATION AND EXTRACTION

     The beans are initially cleaned by mechanical screening.  They are then
cracked and cleaned by aspiration.  This is followed by heat conditioning
in a steam tube drier.  The cracks are flaked by flaking rolls and conveyed
to an extractor.  The oil is removed by continuous countercurrent hexane
extraction.  The flakes are then conveyed to the desolventizer toaster
where the volatile solvent is driven off by jacket and sparge steam.
The vapors are condensed and the liquor pumped to a gravity separator.
The water insoluble hexane is sent to solvent storage and the water dis-
charged to the sewer.  The desolventized and toaster flakes are cooled,
blended and loaded.  The oil-hexane mixture is pumped to distillation
where the solvent is evaporated off and condensed.  The oil is then pumped
to storage.  The condensate water from this process contains some entrained
oil and soluble protein but is not a major source of BODc or fat (See
Section V).

SOYBEAN OIL REFINING

     The refining of vegetable oil may employ a combination of several
processes, depending on the product desired.  These processes include
degumming, caustic refining, subsequent washing, vacuum drying, bleaching,
hardening, post bleaching, filtration and deodorization.

Degumming

     Approximately 2% water is added to the oil to hydrate the gums (phos-
phatides).  On hydration these gums become oil insoluble and are separated
from the oil in a centrifuge.  The gums are then dried to produce lecithin.

     This step can be bypassed; however, it decreases the amount of soap-
stock produced in caustic refining and in the case of soybean oil, produces
a valuable by-product.
                                       5

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        SOYBEANS
           i
                       STEAM
CLEANER
TRASH


CRACKING
ROLLS



SEPARATOR
1
MEATS
\
STEAMER
HULLS


FLAKES ,
\_
FLAKING
ROLLS


               SOLVENT
                                         STEAM
        EXTRACTOR
                    SPENT
                    FLAKES
        —MISCELLA
 DESOLVENTIZER
    TOASTER
                               DUST
       COOLER
         GRINDING  &
          BLENDING
                                                               AIR.
                                      —VAPORS
                        WATER
                    SOLVENT VAPOR:
                 SOLVENT
              EVAPORATORS
 SOLVENT
CONDENSER
                                                             SOLVENT
SOLVENT
STORAGE
ENTRAPMENT
 SEPARATOR
EXTRACTOR
WASTEWATER
                                        SOLVENT  8 WATER
          EXTRACTED CRUDE OIL   %
         (TO STORAGE OR REFINING)
Figure!. Soybean preparation  and oil extraction flow diagram  (typical Lincoln  and  Decatur).

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CRUDE fc
OIL
VYMI C.T\
DEGUMMING
LECITHIN
CAUSTIC SOLUTION '
(Na
DEGUMMED fc
OIL 1
TO
LOADINI
OH) 1
CONTINUOUS
REFINING
r%
ACID TO OIL
STORAGE
SOAPSTOCK ^

ACIDULATION
ACID-
kl ^ WATER
NaOH

NEUTRA
^* ATION
WATER
1 ,
SOAPSTC
WASHIN


irK
/VI\
G
r
LIZ- TO WATER
TREATMENT
UDADING


CLAY

^
^ VACUUM
DRIER UL
.EACHING
SPENT CLAY
(TO LANDFILL)
CLAY
1
1 _ POST
BLEACHING
CATALYST AND
HYDROGEN J

l
H
""•(HYC
AR
)R(
DENING
X3ENATION)


UNHARDENED OIL
(TO LOAI


FILTRATION




DING)
k HARC
STEAM
*
DEODORIZER


FILTRATION
SOAPSTOCK
WASH WATER


FILTER CAKE
(TO LANDFILL) *
)ENED OIL 1

FILTRATION
FINISHED
OILS
(TO STORAGE)
  SPENT CLAY
(TO LANDFILL)
FILTER CAKE
DEODORIZED
DISTILLATE
  FILTER  CAKE
(TO LANDFILL)
               Figure 2.  Oil refining flow diagram.

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Caustic Refining

     Soybean oil is primarily triglyceride with approximately 0.5% to 1.0%
free fatty acids.  The object of caustic refining is to convert the free
fatty acids to water soluble soaps and then to remove them by centrifugation.
A 12% sodium hydroxide water solution is mixed with the oil.  The water soap
solution and oil is then separated in a centrifuge.  The chemical equation
for this reaction is:

                        0                  0
                    R-C^   + NaOH      R-Qf      + H.O
                       N)H                VNa+

     The water soap solution (called soapstock) is pumped to acidulation
where sulfuric acid is added on a batch basis to convert the soaps to fatty
acids.  The fatty acids are insoluble in water and float to the surface.
The mineral salts and any water soluble material remains in the water layer.
The water layer is neutralized and discharged to the waste treatment
facilities.  The chemical equation for this reaction is:
                 2 R-C(        + H-SO,      2 R-(    -i- NaSO.
                      VNa+

Water Wash

     The oil from caustic refining contains trace amounts of soaps and
sodium hydroxide.  Condensate water is added to the oil and agitated to
remove this residual material.  The oil and water from this process is a
weak (\% to 3%) soap solution with a relatively high pH.

Vacuum Drying

     The oil from water washing contains trace amounts of water that can
blind the filters in subsequent filtration operations.  In vacuum drying
the oil is heated under a vacuum of 28" Hg to remove this trace moisture.
There is no significant waste stream from this process.

Bleaching

     Trace amounts of color bodies are removed by absorption onto activated
bleaching clay.  The clay and oil are slurried and heated under vacuum.
The clay is then removed in pressure filters and disposed of in the muni-
cipal landfill.

Hardening

     Hardening is employed to raise the melting point of the oil for use in
shortening or margarine manufacture.  This is done by the addition of hydrogen
to unsaturated oil molecules over a nickel catalyst.  The catalyst is
                                       8

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blended with the oil and heated.  The hydrogen gas is then bubbled through
the mixture.  The degree of hardening is determined by the temperature,
pressure and quantity of hydrogen gas added to the reaction.   The catalyst
is filtered out of the oil after the reaction is complete.  No significant
wastewater is generated by hydrogenation.

Deodorization

     The purpose of deodorization is to remove volatile impurities that might
cause flavors and odors.  This is done by steam distillation at temperatures
of 425°F to 475°F and 3 mm Hg absolute pressure.  The high temperatures
are obtained with a dowtherm boiler heating system.  The vapors are pulled
off through the vacuum system.  (See Figure 3)  A recycle deodorizer dis-
tillate scrubber removes the bulk of the organic material from the vapor
(99%+).  Excess distillate is pumped to storage and sold as a valuable
by-product.  Deodorizer distillate is a valuable source of a-tocopherol
(Vitamin E).  The remaining vapors, primarily steam, are condensed in the
water scrubber along with any remaining organic material and drain to the
greasy cooling tower hot well.

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OIL IN
        -Lr_J
         I-   I
                COOLER
                           SCRUBBEF
                         JWATER
                 TO DEODORIZER
                 DISTILLATE TANK


                 OIL OUT
      SPARGE STEAM
-£
                                                                  GREASY
                                                                  COOLING
                                                                  TOWER
                                                BAROMETRIC
                                                CONDENSER
            V
                                                                     TO HOT1
                                                                      WELL
                       Figure 3.  Deodorization flow diagram.

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                                  SECTION V

                WASTEWATER SOURCES, ANALYSIS, AND QUANTITIES


     All analyses except COD were conducted according to the test procedures
given in Standard Methods for Analysis o;F Water and Wastewater, 12th Edition.
The test procedure for COD is given in Appendix C.  This modified procedure
was used because of the shorter reflux time and because it is more closely
related to BOD5 than the standard method.  This modified COD will be denoted
by quotation marks.  Figure 4 compares the COD analysis to the BODs analysis.

     Flows and wastewater analysis for each wastewater source are presented
in Figure 5.

     The condensate water is generated in heating coils and jacket steam
throughout the refinery.  It is generally hot, clean water and most of it
is being recycled as washwater in the refining step.

     Washwater generated in the oil washing step is high in BOD and fat
primarily because of dissolved soaps.  The stream will contribute 1000
to 5000 Ib per day of fat or BOD5 to the sewer load.  If the oil is not de-
gummed before caustic refining, some water soluble phosphatides will be
removed in this step and will cause higher loads.  This is generally the
case when corn oil is being processed.

     Floor washings are highly variable for obvious reasons.  It is charac-
terized by high temperature and high pH because of the washing equipment
and soaps.

     Greasy cooling water can be a major source of BODs depending on the
operation of the deodorizer scrubber and atmospheric conditions.  (See
deodorization description Section IV)  Any organic material that passes
through the scrubber becomes emulsified in the greasy water in the vacuum
system.  The greasy cooling tower dissipates the heat of condensation of
the steam primarily by evaporation of the greasy water.  In cold weather
the water loses more heat by convection which decreases the amount of
evaporation necessary.  When the amount of water entering the tower via
steam condensation is greater than the wind drift plus evaporation, it
becomes necessary to blow down the tower to the sewer.  The organic material
in the water is primarily short chain free fatty acids.  Typical COD values
range up to 3000 mg per liter.  For an overflow of 30,000 gal per day,
750 Ib of COD would be discharged to the sewer based on 3000 mg per liter
of fat.
                                      11

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                                   ""
                   BODg » 354- 1 .01  COD"
                   95%  CONFIDENCE LIMITS
  5000 —
1000     2000      3000
                                               4000
                       "COD" mg/l
Figure 4.  BOD and COD correlation for total West plant effluent.
                            12

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                                                    REFINERY
CO
                                              134,000-183,000 GPD
                                                 SKIMMER
                                                 CLARIFIER
0x5: rn
r~ CD
H
OD m
O2
~O rn
3 O
*s

CO
m
CO 6
/: 20,000 -30,000 GPD,
FEWATER CHARACTERS
i
CO
X
m

HO
%5






r x
is
DD H
O rn
P s
o
X
ro
o
0
o
TJ



^
CO
-n
k
L 0-100,000 GPD, -CO
'EWATER CHARACTERIS
CONDENSATE WATER

oH
CO
1
PLANT
CI2 TREATMENT





PROCESS  SEWER
                                                                                                         _l
                     EXISTING SAMPLING AND
                      RECORDING STATION
                                     Figure  5.   Schematic of major wastewater sources,

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     Tank car washings vary from one to four cars per day.   The effluent is
characterized by high temperature, 160°F, and a variable amount of emul-
sified oil.  The BODs can be anywhere from 2000 to 60,000 mg per liter.
(Table 1)

     The neutralized acidulation water flow and COD is highly variable de-
pending upon the amount of flush water being used on the centrifuges and
whether or not the oil is being degummed prior to the refining.  The
phosphatides which would be removed in degumming greatly increase the
strength of the acidulation water due to their water solubility.   Fresh
water can increase the moisture content of the soap from 50% to 95%.
While this does not affect the total BOD5 load, it does reduce the residence
time in treatment facilities and reduces the processing time which is ne-
cessary to get good oil separation.  While the BODs is very high (25,000
mg per liter) for this stream, the fat is relatively low (300 - 500 mg
per liter).  This is the only waste stream from the refinery that is not
composed primarily of hexane soluble material.  A typical day would yield
loadings of 4000 Ib per day BOD and 70 Ib of fat based on 20,000 gal at
a 25,000 mg per liter BODs and 400 mg per liter fat.

     The extraction plant wastewater consists of condensate described in
the process section.  At 150,000 gal per day and 300 mg per liter BOD,
this stream contributes only 375 Ib per day of BOD.  The temperature is
high (180°F) and the pH is near neutral (6-8).  Flows were estimated
from process design requirements.  (Table 2)
TABLE 1.  CHARACTERISTICS OF REFINERY WASTEWATER COMPONENT STREAMS GRAB
          SAMPLES
  Source

Acidulation
Tank

Acidulation
Tank

Acidulation
Tank (Settled
Sample)

Tank Car
Washing (Crude
Oil)

Tank Car
Washing
(Hydrogenated)
      Sampling
 Date          Time
9-09-69
9-11-69
4 p.m.
9-11-69     9:30 a.m.
            Wastewater Characteristics
           COD (mg/1)   pJi   Temp.  (°F)
26650     5.6   1150-160
             29220     4.6    150-160
             24760     5.0    150-160
            2-6 p.m.
9-11-69    (Composite)       60400     6.0    150-160
9-11-69    (Composite)
              4655     6.1    150-160

-------
TABLE 1.  CHARACTERISTICS OF REFINERY WASTEWATER COMPONENT STREAMS GRAB
          SAMPLES (Continued)
  Source
     Sampling
Date          Time
                                              Wastewater Characteristics
                                             COD (mg/1)   pj]_   Temp. (°F)
Tank Car
Washing
(Hydrogenated)     9-16-69    (Composite)
                                                2100
                                     6.7    150-160

TABLE 2.
EXTRACTION
PLANT LOADING

Sample
Date
Extraction Plant
9-24-69
9-26-69
9-30-69
10-01-69
10-02-69
Average
BOD,
(mg/T)

325
496
370
360
370
384
Estimated Flow
(GPD)

150,000
150,000
150,000
150,000
150,000
150,000
                                    15

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                                 SECTION VI

                         PRIMARY CHEMICAL TREATMENT
     The initial objective was to determine by laboratory experimentation
whether a chemical pretreatment of any waste water stream was feasible.
Several chemicals, including polymers, polyelectrolytes, sodium chloride and
calcium chloride were used.  Calcium chloride was found to be the most
economical and efficient coagulant at dosages of approximately 0.25% by
weight.  The equation for this reaction is:


               2 R-Qf      + Ca++      2 Na+ + (R-G(   ) Ca++
                    N0-Na+                          0-2

     The normal pH of the washwater was in the range of 10.5 to 12.5 and
while some separation was accomplished at this pH, a more rapid and effective
coagulation and separation occurred at a lower pH.  After the addition of
the calcium chloride to the washwater, an adjustment to the 5 - 6 pH range
with sulfuric acid greatly enhanced the speed of flotation and made the
floe more dense.  Table 3 shows COD reductions using this chemical treatment
on the washwater.  The average reduction in COD was 91.7%.
TABLE 3.  LABORATORY WASHWATER COD REDUCTION BY CALCIUM CHLORIDE TREATMENT*
          AND pH ADJUSTMENT


                    COD Before Treatment        COD After Treatment
        Test        	(mg/1)	              (mg/1)	

          1                25142                       2280
          2                26560                       3750
          3                39000                       3176
          4                51000                       3276
          5                29366                       2061
          6                44662                       4008
          7                17766                        934

       Average             33356                       2783

       *Calcium chloride added was 0.25%.
       +Average reduction was 91.7%.
                                      16

-------
     Because of the success of the laboratory investigations,  primary treat-
ment units were installed at all ADM refineries.   Figure 6 shows  the  plant
layout used for this system.  The washwater from the water wash centrifuges
is discharged into the 5500 gal tank on a continuous basis.   Calcium  chloride
is added by a chemical feed pump and a roto-meter was installed to insure
proper proportioning.  The residence time in the 5500 gal tank is dependent
upon the rate of refining and the amount of floor washings being  discharged
to the system.  Because of this, some of the floe is usually recovered in
sedimentation tanks later in the system.  Acid is added to the second tank
to increase the density of the floe and to increase the rate of the rising
flocculated soaps and oils.  The effluent from this tank is pumped to an
oil skimmer located outside the refinery.  The recovered soaps and oils
are pumped to soapstock storage and acidulated.

     Table 4 shows the average Decatur East BODs figures for water discharged
to the municipal sewer for May 1968 before the calcium chloride treatment
was installed and May 1970 after the calcium chloride treatment was installed.
No acidulation is done at Decatur East so the 93.3% overall reduction is
indicative that the process is as effective as expected from laboratory
studies on washwater only.  Overall BODr was reduced at the West  Plant by
71%, the difference being due to acidulation.  (See Table 14,  Section VIII)

     Part of the original grant agreement was to investigate a washwater
recycle process with financing from the United States Department  of Agricul-
ture.  The washwater would have been recycled through an ion-exchange unit
to convert the soaps to free fatty acids.  The grantee submitted  a proposal
for $45,000 for a pilot unit which was rejected.  Development of  the  calcium
chloride treatment had minimized the importance of the ion-exchange process
so the project was dropped.
TABLE 4.  WASTEWATER BOD5 BEFORE AND AFTER CaCl2 TREATMENT INSTALLATION:*
          EAST PLANT DISCHARGE TO MUNICIPAL SEWER
                       BOD5, May 1968,        BODs, May 1970,
                       Before CaClz           After CaClz
    Test                  (mg/1)	          (mg/1)

      1                    1340                    335
      2                    1620                     70
      3                    1270                     30
      4                    1730                    170
      5                    2710                    380
      6                    2650                    100
      7                    2720                    245
      8                    2350                    125
      9                    1595                     70
     10                    2250                     50
                                       17

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TABLE 4.  WASTEWATER BODs BEFORE AND AFTER CaCl2  TREATMENT INSTALLATION:*
          EAST PLANT DISCHARGE TO MUNICIPAL SEWER (Continued)



Test
11
12
13
14
15
16
17
18
19
20
21
22
23
24
25
26
27
28
29
30
31
Average
BOD5, May 1968,
Before CaCl2
(ma/1 )
2055
2710
5200
3620
2100
2100
2100
2100
2100
2100
2100
2100
2100
2070
1900
2100
3610
3300
2590
2360
2460
2358
BOD5, May 1970,
After CaCl2
(mg/1 )
155
680
545
85
155
90
80
100
25
55
25
100
85
105
55
40
25
85
90
50
620
156
     *Reduction in 6005 was 93.3%.
                                     18

-------
, CaCI2
 .1600
   GAL.
                      LARGE LINE 6
           OIL- CaCI2
              5500 GAL.

  •WASHWATER
  WATER
OIL- CaCI,
                                H2S04
1 ...
s.
1
> f
2000 GAL.
TO SOAPSTOCK _



TO OUTSIDE
TREATMENT
TO  SOAPSTOCK
                       Figure 6.   CaCl2 water treatment flow sheet.

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                                 SECTION VII

                    TREATABILITY STUDIES AND DESIGN BASIS
     While chemical treatment of the washwater from the refineries resulted
in an overall reduction in the total waste stream from approximately
50,000 P.E. to 20,000 P.E., there was still a problem resulting from other
wastewaters in the refinery complex which did not respond as readily to
the calcium chloride treatment.  Further studies were needed to reduce the
organic load to within acceptable limits.

     A consulting firm was retained to assist in the investigation of
secondary chemical treatment and to design a treatment process based on these
investigations.  At the same time, the grantee was to investigate the pos-
sibility of treatment with air flotation and process modifications to reduce
the waste load.

GAS FLOTATION STUDIES

     Laboratory studies indicated that finely dispersed gas bubbles produced
by electrolysis will rapidly remove most suspended solids from a waste stream
and materially reduce the BOD.

     Two grids consisting of an anode and cathode were immersed in the bottom
of a chamber and low voltage current was passed between them.  Electrical
current was supplied to the grids with a 20 ampere rectifier.  A direct
current of approximately 2-5 volts and 4-8 amperes was introduced to the
grids which were one half square foot in area.  Hydrogen was generated at
one grid and oxygen at the other in the form of very fine bubbles evenly
distributed over the area.  As the bubbles rose, they attached themselves
to the suspended solids and entrained oils and floated them to the top.

     With this procedure, settleable solids as well as suspended solids
were floated to the surface.  Satisfactory results were usually obtained within
fifteen minutes.  (Table 5)  The data obtained from these experiments showed
a reduction of organic loading of approximately 50%, from 7021 to 3231
mg per liter, beyond the results obtained with the primary treatment which
consists of the already outlined calcium chloride system.
                                       20

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           TABLE 5.  LABORATORY COD REDUCTION WITH GAS FLOTATION
Material
Greasy Water
Wash water
Skimmer Effluent


Water to Sanitary
District
Test
1
1
1
2
3
1
2
Before COD
(rag/1)
3005
29,019
1,606
2,565
2,850
1,140
1,238
After COD
(mg/1 )
248
111
331
1,250
1,650
331
228
     An electrolysis unit was then installed in the refinery skimmer.   One
hundred sixty square feet of 1/2 inch steel floor grate was used for the
anode and cathode.  The grids were placed in the bottom of the skimmer
on bricks approximately 3 inches apart.  Power was supplied by a 1500
ampere Clinton rectifier model number R1512HO-S.  Results seemed to be
promising; however, after a few weeks of operation, the production of gas
bubbles all but stopped.  Upon emplying the skimmer and inspecting the grids,
the cathode was in excellent condition and showed no corrosion; however, the
anode was almost completely eroded.

     Laboratory studies were resumed, and it was found that on prolonged
usage, the anode was indeed eroded while the cathode remained in good condi-
tion.  Studies were then undertaken to find a suitable anode material  to
withstand this eroding effect.

     Anodes of iron, aluminum, titanium, 316 stainless steel, Inconel,
cast iron, monel, nickel and high silica iron were tried without success.
A combination of 316 stainless steel mesh with graphite supports for the
anode gave the best laboratory results.

     A plant scale installation was made with grids consisting of 18 mesh
stainless steel with graphite cross bars.  After a period of two weeks,
the skimmer was drained and the grids inspected.  The anode consisting of
stainless steal and graphite was badly deteriorated.  The stainless steel
mesh was almost completely gone and the graphite had decreased in size
considerably.  The efficiency had deteriorated over the two week period
to a point where few bubbles were observed coming to the surface of the water,
During the first few days of operation, the process worked very well
producing a diffuse bubble blanket.
                                      21

-------
     Another consultant was then employed to develop a workable anode.   This
firm produces material used specifically for this application and they  felt
their material would stand up under the conditions of the process.   The material
consisted of graphite bars 48 inches long, 6 inches wide and 1 inch thick
coated with lead dioxide.  Eight bars were purchased and installed in the
Imhoff tank.  Copper buss bars coated with glyptol, an insulating material,
to prevent corrosion were used to connect the graphite bars.  The coating
did not withstand the corrosion and in two days was almost completely destroyed.

     Graphite connecting bars were then tried and proved to be more successful.
After 1 week of operation, the graphite anodes were badly eroded and began
breaking under their own weight.

     Advances made in other methods of waste control had minimized the  impor-
tance of the development of this system.  At this point, the electrolysis system
was abandoned as being impractical.

SECONDARY CHEMICAL TREATMENT

     Studies were undertaken by the consultant in September 1969 to do  the
following:

1.  Establish the flows and characteristics of the West Plant Refinery,
    Extraction and Subsurface drainage streams.

2.  Do chemical/physical treatability studies on the refinery skimmer effluent.

3.  Develop process design parameters from the above treatability studies.

4.  Propose a treatment facility capable of treating these wastewaters.

    The treatment requirements were set by the Decatur Sanitary District and
    consist of the following:

    a)  For 95% of the time the total Biochemical Oxygen Demand of waste from
        all industry facilities, in the aggregate, shall not exceed 5780
        Ib per day (34,000 P.E.) as any 10-day average nor exceed 7,200 Ib
        per day (42,500 P.E.) as any 3-day average.

     b) The total fats-oils-grease of the waste from the three plants shall
        not exceed 1000 Ib per day as a monthly average, shall not exceed 1,00
        Ib per day for more than 10% of the samples, and shall be less  than
        2,000 Ib per day for 97% of the samples.  The sanitary district reserves
        the right to re-examine these criteria if, after they are met,  phy-
        sical and treatment problems resulting from the grease content  of the
        waste continue.

     Figure 7 is a location plan of the sampling points used in the study.
Grab samples, representative of skimmer effluent, were collected at the lagoon
inlet (sampling point No. 1)  at 2-hour intervals over a period of 3 days
from September 9 to September 12, 1969.
                                      22

-------
SKIM TANK
    O
  PUMP
STATION
            \
TO DSD
             \      FROM  REFINERY

             \
                                                  DULATION
                                                  FACILITIES
       ®
            LAGOONS (TVIO IN SERIES)
                                        ..J
                                          UNDERDRAIN-
                                         OL SEPARATOR
                                                      TO
                                            HOMEWOOD LAKE
    Figure 1.   Treatment flow diagram during water survey.
                              23

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                   TABLE  6.    CHEMICAL  FLOCCULATION  SCREENING  TEST  RESULTS  FOR WEST REFINERY  SKIMMER  EFFLUENT
            Raw Sample,
       Collection
        Date and
          Time	
 Type
  of
Sample
 Characteristics
                                                                     Treatment
 COD
mg/1
PH
       Temp
        OF
   Coagulants	       Coagulant Aid	
Type       Dosage, rnq/1     Type    Dosage, rng/1
Qualitative Observations and Conclusions from Jar
  	Test Results	
         9-9-69
        11:30 a.m.
 Grab
6,400    6.2
                          155
               FeCl3       100  to 1000
ro
                                                     Ca(OH),
                                                      CaCl,
                                             200 to  1000
                                             200 to 2000
                                                      Fe2(S04)3    100 to  1000
                                                 FeCU dosages below 1000 mg/1 did not s^eein to have
                                                 any  significant effect on  breaking the emulsion.
                                                 The  supernatent with Fed, dosages at less than
                                                 1000 mg/1 after centrifugation still was very
                                                 turbid.  1000 mg/1  dosage  gave food floes and
                                                 relatively clear supernatent.  The Fed, treat-
                                                 ment at a dosage of 1000 mg/1 was judgea as
                                                 effective.

                                                 Floe formation was  poor at 200 mg/1 dosage.
                                                 Supernatent was turbid after centrifugation.
                                                 However, 400 mg/1 to 1000  mg/1 dosage gave good
                                                 floes and clear supernatent after centrifugation
                                                 floe formation was  almost  instantaneous.  The
                                                 pH at these dosages valued from  7 to 8.  The
                                                 Ca(OH)2 treatment above 400 mg/1 was judged as
                                                 effective.

                                                 There was no apparent flocculation.  No change in
                                                 clarity after centrifugation, no sludge formed at
                                                 the  bottom.  CaClp  treatment at  all dosages was
                                                 judged as ineffective.

                                                 No flocculation was observed up  to 5000 mg/1
                                                 dosage.  Supernatent was very turbid with very
                                                 slight sludge at the bottom after centrifugation.
                                                 pH was 5.9 at 100 rag/1 dosage and 5.4 at 500
                                                 mg/1 dosage.  1000 mg/1 dosage gave good
                                                 flocculation with clear supernatent after
                                                 centrifugation.  pH was 5.0 Fe-fSOJ, treatment
                                                 at a dosage of 1000 mg/1 was jadgea as effective.

-------
         TABLE  6.   CHEMICAL  FLOCCULATION  SCREENING TEST RESULTS  FOR WEST REFINERY SKIMMER EFFLUENT  (Continued)
Raw Sample
Collection Type
Date and of .
Time Sample
—
Characteristics
COD
mg/1

Treatment
Temp Coagulants
PH

°F Type
A12(S04}3
Dosage, mg/1
100 to 1000
Coagulant Aid
Type

Dosaqe, mq/1
--
Qualitative Observations and Conclusions from Jar
Test Results
Flocculation was very poor up to 500 mg/1
dosage.
ro
         9-9-69
        3:30 p.m.
Grab
19,000   7.5
148
Fed-
200 to  1500
                                                    Ca(OH),
                                           100 to 2000
                                                                                                     supernatent clarity.   However, the results were
                                                                                                     still  poor.  The pH was 5.8 at 100 mg/1  and 5.3
                                                                                                     at 1000 mg/1 dosage.   AlJSO.k treatment was
                                                                                                     judged as  ineffective.
At 200 mg/1 dosage there was  no noticeable effect.
At 300 mg/1 dosage the floes  formed after 10 mins.
Some floated at the top, some settled down.   The
sample was still very turbid.  Centrifugation did
not improve the clarity.  500 to 1500 mg/1  dosage
gave large amount of floes  through out the depth.
Centrifugation gave some sludge at bottom,  some
scum at the top and still  large amounts of floes
throughout the depth, indicating that the mass
density of the floes was same as that of the
wastewater.  pH at a dosage of 500 mg/1 was  6.6
and that at 1500 mg/1 was 40.  The FeCK treat-
ment on this sample was judged as ineffective.

Up to 500 mg/1 dosage there was no significant
change in the sample appearance.  At dosages of
1000 mg/1 and above there was almost instant
floe formation.  However, the supernatent was
still very turbid even after Centrifugation.
The pH at 500 mg/1  dosage was 8 and those at 1000,
1500, and 2000 mg/1 were 10.3, 11.1, and 11.5
respectively.  The Ca(OH),.,  treatment was judged
as ineffective.

-------
          TABLE 6.   CHEMICAL FLOCCULATION  SCREENING TEST RESULTS FOR  WEST  REFINERY  SKIMMER  EFFLUENT (Continued).
Raw Sample
Collection
Date and
Time
Type
of
Sampl e
Characteristics
COO
mq/1
PH
Temp.
°F
Treatment
Coagulants
type
Dosaqe,
mq/1
Coagulant Aid
Type
Dosage,
Qualitative Observations and Conclusions from Jar
mq/1
Test Results .
                                                     CaCl,
CT>
                                                    Fed.
100 to  2000
                                                    Fe2(S04)3    200  to 1500
                                                   y\i2(so4)3     200  to 1000
500

500

500

500
                                                                              DOW
                                                                             N-ll
                                                                              DOW
                                                                             N-11
                                                                              DOW
                                                                             N-ll
                                                                              DOM
                                                                             N-ll
At 200 mg/1  dosage there was no apparent change.
At 500 mg/1  and above there was floe formation.
However, the sample was still  very  turbid after
centrifugation.   In this particular the floes
floated on the top.  The pH at 200 mg/1 dosage was
6.9 and that at 1500 mg/1  dosage was 6.2.  The
CaClp treatment was judged as  ineffective.

Up to 300 mg/1 dosage there were no visible floes.
The mg/1 dosage formed very small floes after a few
minutes.  1000 mg/1 and layer  dosages gave  instant
floes.   However,  the sample was still very  turbid.
Some floes floated to the  top, some settled, and
some still remained in suspension throughout the
depth after  centrifugation. The pH at 200  mg/1
dosage was 7.2 and gradually decreased to 5.7 at
dosage of 1500 mg/1.   The  Fe,(SO/!)0 treatment was
judged ineffective.
                                                                                                                                    J4'3
Similar results as above except that the pH at  1000
mg/1 dosage was 6.5.  A12(SO«), treatment was
also judged ineffective.

Using 4 of these polyelectrolytes along with 500
mg/1 Fed, gave large floes.  However, the results
were judged as no better than Fed, treatment
alone.  This treatment was also judged as in-
effective.

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        TABLE 6.   CHEMICAL  FLOCCULATION  SCREENING TEST  RESULTS  FOR WEST  REFINERY SKIMMER EFFLUENT  (Continued)
Raw Sample
Collection
Date and
Time
Type
of
Sample
Characteristics
COD
mg/1
Temp.
pH °F
Treatment
Coagulants
Type Dosage, mg/1
Coagulant Aid
Type Dosage, mg/
Qualitative Observations and Conclusions
1 Test Results
from Jar
        9-10-69
Composite 3,900
of 2 hr.
grab sample
over 16  hr.
period.
6.2
ro
  Cad,
 Ca(OHf5
Ai2(so4}3
                                                      Fed.
                                                      Fed.
500 to  1500
500 to  1000
500 to  1500
                                            500 to 1000
                                            500

                                            500

                                            500

                                            500
                                      DOM
                                      C-31
                                      DOW
                                      A-23
                                      DOW
                                      N-ll
                                      DOW
There was apparent flocculation.  The floes
settled; however, the supernatant was still
turbid after centrifugation  indicating that
there was no destabilization of the emulsions.
The treatment with these chemicals was judged
ineffective.

At these dosages floes were observed; however,
the supernatent was still  turbid after centri-
fugation.  pH at 500 mg/1  dosage was 5.2 and that
at 1000 mg/1 was 4.6.  This  treatment was judged
ineffective.

Some floes formed.  No clear supernatent after
settling.
Some floes formed.  No clear supernatent after
settling.
Relatively clear supernatent.  However,  still lot
of turbidity after settling.
Considered as less effective than DOW N-ll; however,
better than C-31 and A-23.  The combination of 500
mg/1  Fed, and 5 mg/1 of DOW N-ll marked the best
in this series.  COD was reduced from 3900 mg/1 to
1300 mg/1.  This treatment was judged as effective
on this composite sample.

-------
     Flows were obtained by timing the total duration of pumping over a given
time interval.  Due to some difficulties in recording the flows, it was not
always possible to determine the flow rates and the total flows corresponding
to the time or period of sampling.  Since the effectiveness of the Imhoff tank
located in between the skimmer outlet and the lagoon inlet was considered
negligible, no sampling was done to define its performance.

     Other grab samples from the acidulation facilities, lagoon effluent and
subsurface drainage were collected from sample points 3, 4, and 5, respectively.
Flows for these discharges were estimated from process design requirements.
Results of this survey in conjunction with data generated by ADM is presented
in Section V and will not be.presented here.

     The wastewater survey revealed that BOD (as approximated by COD) and oils
was the major problem in the effluent from the West Plant.  Further, comparisons
of the three major sources of wastewaters revealed that the refinery wastewaters
contribute over 80% of the organic load.  Consequently, emphasis was placed
on the chemical/physical treatment of the refinery wastewaters for BOD5 and
oil reduction.

     Since results of the analysis of lagoon effluent samples showed little,
if any, equalization of other significant or consistent improvement in quality
over the skimmer effluent samples, major emphasis was placed on the treatment
of the refinery skimmer effluent wastewaters.  Grab and 24-hour composite
skimmer effluent samples obtained during the problem definition survey were
evaluated to determine the most effective and economical process for reduction
of BODs and oils.  Grab versus composite samples were tested to determine the
necessity and advantages of equalization prior to further treatment.  Laboratory
tests included pH adjustment, activated carbon absorption, inorganic and or-
ganic chemical coagulation for emulsion destabilization, and gravity settling
and air flotation for separation of chemical floes and oils.

     Coagulation screening tests were performed on grab as well as composite
samples of skimmer effluent for refinery wastewater.  These studies were
qualitative in nature and were conducted to determine the types of coagulants
best suited for the wastewater and to investigate the need for an equalization
basin.

Grab Samples

     Fifty-mi Hi liter samples were used for these summary tests.  Different
coagulants with and without different polyelectrolytes were screened.  After
coagulant(s) addition, the samples were slowly stirred and observed for floe
formation and supernatant clarity.  The coagulant which did not form floes in
30 minutes and/or did not produce a clear supernatant were not evaluated further.
The results of these studies are presented in Table 6.  Although not shown
in Table 6, the results of varying wastewater pH with acid and lime did not
produce a significant reduction in COD or improvement in wastewater clarity.
Also tried and found not effective was the use of activated carbon—tried
along, at various adjusted wastewater pH's, and in combination with several
coagulants.  No benefit was observed to justify the increased cost of this
chemical absorbent.

                                      28

-------
     It may be noted that the coagulants that worked on one grab sample
(9/9/69 - 11:30 a.m.) did not work at all on the other (9/9/69 - 3:30 p.m.).
Also, it may be noted that in some cases the floes settled, and in the others
they floated.  These results indicate that for unequalized samples one single
approach or solution may not consistently work on the skimmer effluent waste-
water .

Composite Samples

     At this point the same coagulants were tried on the composite samples  of
the skimmer effluent.  The results (presented in Table 6) were very encouraging.
The combination of ferric chloride (FeCIs) and calcium hydroxide (Ca(OH)2)
seemed to produce the best and most consistent results.  This treatment combina-
tion was subsequently quantitatively investigated for COD and oil removal.

     Quantitative studies on coagulation were performed on seven 24-hour compo-
site samples.  These samples were obtained by continuous collection of the
wastewater from the discharge side of the skimmer inlet pump.  The composite
samples were approximately at room temperature due to a loss of heat on standing,
whereas the temperature of the wastewater going to the skimmer varied over  a
range of 110° to 155°F.  In order to simulate composite skimmer effluent,
the samples were mixed well and allowed to stand for 30 minutes and the top
oil layer was skimmed off.  The subnatant was used for the studies.

     The results of the composite sample coagulation studies are presented  in
Table 7.  Quantitative performance was judged on the basis of COD alone with
simultaneous qualitative visual inspection of floe settleability and super-
natant clarity.  The results indicated that the combination of 100 mg per
liter FeCl3 plus 300 to 500 mg per liter Ca(OH)2 generally gave the best
results.  Increasing the FeCls dosage to 200 mg per liter did not give any
better results.  In fact, in many cases, the floe settling rate was observed
to be slower.

     The variability of the 24-hour composite treated skimmer effluent COD's
are presented in Figure 8.  These results show that for the present refinery
skimmer effluent wastewater characteristics, FeCl3 and Ca(OH)2 coagulation
followed by sedimentation would reduce COD's to equal to or less than 850
mg per liter for 50% of the samples, and equal to or less than 1,500 mg per
liter for 90% of the samples.  This represents approximately 65% COD reduction
on the average.

     At the time of these investigations no specific limits for fats, oils
and greases (fat) were imposed by the municipality on the effluent.  Hence,
in order to avoid an excessive analytical work load on the personnel, only
four samples of raw and treated skimmer effluent were analyzed for fat.
The results indicated that the skimmer effluemt FOG can be substantially reduced
by Fed3 and Ca(OH)2 coagulation followed by gravity sedimentation.  The
maximum and minimum fat concentrations of the treated skimmer effluent were
266 mg per liter and 10, respectively.
                                       29

-------
                TABLE 7.   CHEMICAL FLOCCULATION  RESULTS  OF SAMPLES OF  WEST  PLANT REFINERY SKIMMER EFFLUENT
CO
o
Raw Wastewater ^
Characteristics Chemical Dosage

Date of Hours
Sampling Composited "COD"
9-12-69 24 3048






9-14-69 24 1682





Fed,
Oil pH mg/r
2155 6.3 100
100
100

200
200
200
635 6.5 100


100
100

Ca(OH)
mq/1 2
200
300
400

200
300
400
200


400
600
Treated Wastewater
Characteristics


mg/1

—
—

__
—
794
572


568
620
"COD"
%
Reduction
„
--
—

__
68.5
73
66


66
63


pH
6.3
—
—

6.2
6.4
--
7.2


7.4
7.5

Qualitative Observations and Conclusions
from Jar Test Results
Very poor flocculation and very poor
settling. Good flocculation. Very slow
settling floes. Treatment considered
effective.
Results no better than above. However,
larger sludge volume. Treatment con-
sidered effective.
Good flocculation, floe settling slow.
Many floes stayed in suspension. Clear
supernatant.
Almost instant floe formation. Good
flocculation. Floe settling very good.
                                                     200
                                                     200
                                                     200
200
400
600
673
594
60
64.5
      Very clear supernatant.   Treatment con-
      sidered effective.

6.7   Good flocculation.  Floe settling slow.
      Many floes still in suspension, clear
      supernatant.

6.8   Almost instant floe formation.  Good
7.0   flocculation.  Floe settling very good.
      Very clear supernatant.   Floes judged
      to be less dense than with  100 mg/1
      Fed, + comparable CafOH)^  dosage.
      Treatment considered effective.

-------
TABLE 7.   CHEMICAL FLOCCULATION RESULTS OF SAMPLES OF  WEST PLANT REFINERY  SKIMMER EFFLUENT  (Continued)
Raw Wastewater
Characteristics Chemical Dosage
Date of 'Hours
Sampling Composited "COD" Oil
9-15-69 16 2523 842



9-16-69 24 1629








9-17-69 24 2155



Fed,
pH mg/r
6.2 100

100
100
6.2 100

100
100

200

200
200
8.2 100
100
100
100
Ca(OH)2
mg/1
200

300
400
200

300
400

200

300
400
200
300
400
500
Treated Wastewater
Characteristics
mg/1
846

678
762
1051

835
851

_ _

794
867
_ _
--
-_
1787
"COD"
I
Reduction
66.5

73
69.5
35.6

48.7
47.8

__

51.3
47
„_
—
__
17
PH


	
—
6.7

7.0
7.5

6.6

6.7
6.8
	
—
..
7.1
Qualitative Observations and Conclusions
from Jar Test Results
Good flocculation. Floe settling slow.
Clear Supernatant.
Good flocculation. Floe settling very
good. Clear supernatant.
Floes not well defined. Poor f'loc-
culation. Supernatant turbid.
Very good flocculation. Very good
floes. Floe settling very good.
Very good supernatant.
Floes not well defined. Poor floc-
culation. Supernatant turbid.
Good flocculation. Loose floes. Floe
settling slow. Clear supernatant.
This sample was not considered normal
by ADM. It rained heavily on this day.
pH of raw wastewater was adjusted to 6.2
with addition of H9SO,. The oil liberate!
                                                                                    was skimmed off before conducting test.
                                                                                    CaC(OH)2 dosage of  400 mg/1 and 500 mg/1
                                                                                    along wfth 100 mg/1 Fed, gave good
                                                                                    flocculation and clear supernatant.
                                                                                    Floes settled fast.  However, COD
                                                                                    reduction was poor.

-------
       TABLE  7.   CHEMICAL  FLOCCULATION  RESULTS OF  SAMPLES OF WEST PLANT REFINERY  SKIMMER EFFLUENT  (Continued)
CO
ro

Raw Wastewater
Characteristics

Date of Hours
Sampling Composited "COD" Oil pH
9-18-69 24 4993 ~ 5.6




9-19-69 24 2050 266 5.8




Chemical Dosaqe

Fed,
mg/13
100
100
100
100

100

100
100
100

Ca(OH)?
mg/1 *•
200
400
600
800

300

400
500
600
Treated Wastewater
Characteristics


mg/1
..
—
4047
..

783

804
840
--
"COD"
%
Reduction
— —
—
19
--

61.5

61
59
*•""


PH
«•_
—
7.1
—

6.2

7.0
8.2
8.3

Qualitative Observations and Conclusions
from Jar Test Results
Flocculation test gave negative results.
Floes were almost throughout the depth.
No settling, no flating of floes.
Dow N-ll at 1 to 2 mg/1 dosage along with
those coagulants also did not help.
Small floes. Slightly turbid super-
natant. Floe settling good.
Small floes. Clear supernatant. Floe
settl ing very good.

        Flocculation Procedure:  500-ml sample in 1 liter beaker, chemical added; 2 minutes  rapid mix at 100 rpm;  15 minutes flocculation at 40 rpm;
                              supernatant analyzed after 15 minutes  settling.

-------
   7000
   5000
 £ 4000
 Q
 O
 O
   1000
 200 —
   6000   gl80
          CD
Q
Z
w
o
   3000   -120
   2000   -noo
          o
   80
                               A   FLOW 	
                               O   COD  	
                    I      I   I    I   I   III     II
                    10   20  3040506070  80   90   95

                               PERCENT OF TIME
          FLOW AND COD ARE EQUAL TO OR LESS  THAN
                        GRAPH VALUES

Figure 8.  West plant refinery skimmer effluent variability of 24 hr
         composite COD and flows.
                             33

-------
                       TABLE  8.    LABORATORY  SETTLING  TEST  RESULTS  OF  REFINERY SKIMMER EFFLUENT
Suspended Solids and
Sludge Production
24-hr Composite Sample






CO
•£»








Collection
Date
(Ending)
9-13-69



9-14-69

9-15-69

9-17-69
9-19-69





COD, mg/1
3,048



1,682

2,523

2,155
2,050





OH, mg/1
2,155



635

848

--
266





Coagulant
Fed 3, mg/1
100



100

100

100
100




Treatment

Dosage
Ca(OH),, mg/1
400



400

400

500
400




Settled Supernatant Duality
Laboratory*
Overflow Rate
gas/sq ft/day
1,200
600
400
200
400

400

200
1,200s
600
400
300
125


mg/1
1,314
946
998
1,050
557

778

1,734
840
820
825
794
778

COD
% reduction
57
69
67
65.6
67

69

19.5
59
60
59.5
61
62


mg/1
__
--
266
"
97

131

•-
__
_-
10
._
--

on
% reduction
	
--
87
--
85

85

--
	
—
96
--
--
Sludge
Volume
mg/1
of Waste
70
65
50
50
43

60

105
105
80
65
57
43
Suspended
Sol Ids
after
Chemical
Treatment, mg/1
904



622

884

922
..
--

--
--


Remarks and Observations
Clear supernatant. Turbidity
judged as 10 Jackson Turbidity
Units (JTU).

Visual inspection of the sus-
pension during the test indi-
cated that similar removal could be
obtained at overflow rates of 600 gpd/sq
Clear supernatant.
Clear supernatant. Turbidity judged as
JTU.













ft.

10




 Samples were pretreated 1n the settling cylinder Itself, using  the Indicated coagulant dosages and flocculated for 15 minutes prior to settling.  These
 coagulant dosages were judged as optimum by jar test analysis.  The samples were at room temperature.
*One-L1ter graduated cylinder settling test, (14" water depth).
'six-Liter cylinder settling test, (14" water depth),
tin all the tests a thin scum layer was observed floating on the top.  This was excluded from the supernatant sample.

-------
     A series of laboratory-scale settling tests were performed at  room
temperature using skimmer effluent wastewater treated with the optimum coagulant
dose of ferric chloride and calcium hydroxide (determined by a modification of
the previously described screening procedure).  A summary of results  is  presented
in Table 8.  A small percentage of solids floated to the liquid surface  in all
the coagulation and sedimentation studies, indicating the need for  some  type
of skimming equipment in the clarifier.

     The relationship between clarification overflow rate and the treated
effluent COD is presented in Figure 9.  Generally, suspended solids removal
is used as a criteria in determining the design overflow rate for a sedimenta-
tion tank.  However, in this particular case, with the removal of flocculated
wastewater BODs being the prime consideration, supernatant COD was  used  as a
criteria to determine the overflow rate.  The data shown in Figure 9 is  typical
of the several settling tests run and is summarized in Table 8.  Interpretation
of the laboratory overflow rates indicated that in most cases a clarifier over-
flow rate of approximately 750 gal per square foot per day will produce  an
effluent with a minimum COD.  A scale up adjustment factor of 1.5 was applied
to the laboratory observed overflow rate to account for hydraulic turbulence,
temperature induced turbulence, inlet and outlet losses, etc.  In one case
the floe settling was very rapid and a laboratory overflow rate as high  as  1200
gal per square foot per day also produced very good supernatant.  For design
purposes, however, an adjusted overflow rate of 500 gal per square foot  per
day was used.

     The effectiveness of chemical coagulation of grab samples taken from the
skimmer outlet at different times of day was not consistent, indicating  that
effective equalization is necessary for reliable treatment.  The chemical
coagulation of 24-hour composite samples from the skimmer effluent, in most
cases, gave good results, indicating that 24-hour equalization should be sufficient.

     Chemical coagulation of equalized skimmer effluent  (using a combination
of ferric chloride and calcium hydroxide) followed  by flocculation and sedi-
mentation reduced the COD to 850 mg per liter or less in  50% of the samples  and to
about 1,500 mg per liter or less in 90% of the samples.   The behavior of two
samples taken on September  17 and 18,  1969 stresses the  importance and the need
for dependable in-plant treatment with calcium chloride,  and effective oil
separation and removal in the new in-plant and the  existing refinery wastewater
effluent skimmers.  A summary of the  investigative  results  is  given in Table 9.
                  TABLE 9.   SUMMARY  OF INVESTIGATIVE  RESULTS
      Item         .                                  Amount

 Equalization:
    Detention Time,  Hours                             24
                                     35

-------
               TABLE 9.  SUMMARY OF INVESTIGATIVE RESULTS (Continued)
     Item                                          Amount
Coagulation:
   Ferric Chloride (FeCl^) Dose, mg/1                100
   Calcium Hydroxide (Ca(OH)2) Dose, mg/1
      Minimum, mg/1                                 300
      Average, mg/1                                 400
      Maximum, mg/1                                 500

Clarification:
   Overflow Rate (lab), gal/sq ft/day               500
   Average COD Reduction, %                          65
   Average Fat, Oils, and Greases Reduction, %       85

Treated Effluent:
   COD, mg/1, 50% Probability Value                 850 (1,300)*
              90% Probability Value               1,500 (2,200)
   Fats, Oils, and Greases, mg/1                 10-270 (10-400)

Clarifier Sludge
   Minimum Solids Concentration, %                    1
   Maximum Solids Concentration, %                    2
   Average Sludge Production, % of
      Wastewater Flow                                 6


*Figures in parenthesis indicate future production rate.

General Basis of Design and Recommended Process

     The design of the treatment facilities is based on the estimated 90%
probability-of-occurrence value of future West Plant refinery skimmer effluent
flows and loadings.  Chemical dosages are based on the results of laboratory
investigations using compsited skimmer effluent samples.   A scale-up factor
of 1.5 has been applied to the results of laboratory overflow rates to obtain
design overflow rates for the clarifiers.  Flocculator-clarifier units are
provided in duplicate for maintenance and operating flexibility.

     The design of chemical feed systems is based on the requirement that
minimum supervision and operating manpower will be available.  Hydrated lime,
instead of pebble lime, will be used.   However, since the average lime requirement
is only 725 Ib per day as Ca(OH)2, the additional cost of hydrated lime over
pebble lime is negligible.  The capacities of the lime feeder, lime mixing
tank, and transfer pumps are designed such that a whole day's lime slurry re-
quirement can be prepared in one to two hours during the day shift.  The lime
slurry storage tank is designed to store three days' average supply of lime

-------
                      24 HR. COMPOSITE  SAMPLE
                       A 9-12-69  TO 9-13-69
                       O 9-18-69  TO 9-19-69
                                            TREATMENT CONSISTED OF OPTIMUM
                                            DOSAGE OF FeCI3  AND Ca(OH)2
                                            COAGULANTS
CO
         CO
         "U
         m
5
m
-I
 s
O
o
1400

1200

1000

 800

 600

 400

 200

   0
                        I     1     I    I     I     1     [     I     I    I    I     I
                                                         8
                                                          10   II
                                                              12
                           OVERFLOW  RATE,  HUNDREDS OF GAL/DAY/SQ. FT.
                 Figure 9.  West plant refinery treated skimmer effluent settling test results

-------
at a 10% slurry concentration.  This will also allow the storage of weekend
lime slurry feed requirements, and thereby minimize operator attention over
the weekend.  The capacity of the lime dry storage hooper is designed for 1.5
times the capacity of a delivery truck.  This provides approximately 75 days'
storage at the average rate of use.

     Ferric chloride will be purchased, stored, and fed in liquid form.  Acid
resistant materials will be used through this system.

     Equalization of skimmer effluent is necessary to level out the variability
of flows and loadings prior to chemical treatment, as was demonstrated during
the treatability survey.  A portion of the existing lagoon will be modified to
serve as the equalization basin.  The remainder of the existing lagoon will
provide a second basin to serve as emergency storage for excessive surface
runoff, production leaks, and spills and other miscellaneous flows.  These
accumulated wastewaters will be bled into the equalization basins for further
treatment prior to discharge to the municipal sewer system.

     The design assumes that the necessary changes in the refinery effluent
pumping and skimming facilities, as previously discussed, will be completed,
and that these units will remain as part of the proposed treatment scheme.
The present Imhoff tank and lagoon will be abandoned or modified for use in
proposed new treatment facilities.  Since the refinery wastewaters are pre-
sently receiving CaCl2 treatment, no further adjustments were made to account
for the changes when this treatment is moved in-plant.

Description of Proposed Facilities

     The schematic flow diagram for the proposed treatment facilities and
the preliminary plot plan are shown in Figure 10.

     The wastewater from various refinery sources after being collected in the
existing sump, will be pumped to the existing skimmer, where free floating
oil present in the wastewater will be removed.  The skimmer effluent will then
flow by gravity to the equalization basin (T-|), which will provide an equaliza-
tion period of one day at design flows.  Manually-diverted influent or any
overflow from the equalization basin will be stored in an emergency storage
basin (TIQ) with a capacity of 180,000 gal and will be pumped back (via
Pump PIS) to the equalization basin at a manually controlled rate during
the periods of low in-flows, for retreatment.  Under normal conditions, the
emergency basin will remain empty.

     The equalized skimmer effluent will be pumped (using two centrifugal
pumps, P-J, P2) to the flash mix tank.

     A constant flow rate, adjusted manually according to the level in the
equalization basin, insures more uniform operation and performance of the
downstream facilities, and simplifies control of the coagulants feeding systems.
Lime and ferric chloride will be added automatically in proportion to the waste-
water flow.  Lime will be fed from a recirculated storage tank system with
a flow-activated control valve.  Ferric chloride solution will be fed directly
                                     38

-------
CO
    HYDRATED LIME
(LI) SILO 12x20'
                                                                             (LV> _ (LLCO)
                                                                                *X—|   {—*»TO DSD
                                                                       STORAGE 11
         LIME MIX
         TANK
          LIME CONVEYOR
                                                                  SPLITTER
                                      FLASH
                                      MIXER
                       (LLCO)   (FIG!
                      SKIMMINGS
                       -HOLD
                        TANK
 EQUILIZATION
EMERGENCY DISCHARGE
                                                    FLOCCULATOR
                                                    CLARIFIERS
                                           HOLD
                                           TANK
                                           T-5
                                 AcoN
               STORAGE      .    ACIDULATION
              iBASIC    T-IO  EMERGENCY OVER
                            FLOW TO DSD
HLA
LLCO
FR
FT
F 1C
TS
HIGH LEVEL ALARM
LOWLEVEL CUT OFF
FLOW RECORDER
FLOW TOTALIZER
LI

NC
NO
FLOW INDICATOR CONTROLLER
TORQUE SWITCH
LEVEL INDICATOR
LOW LEVEL INDICATOR
NORMALLY CLOSED
NORMALLY OPEN

                                                                 ACIDULATION
                                                                                ADM
                                                                             FACILITIES
                                Figure 10.  Proposed treatment facility.

-------
from the storage tank by a variable-speed metering pump controlled by the
wastewater flow.  The lime and ferric chloride feed systems will  be housed
in a small control building.  The lime storage bin will be located outside
the building.

     From the flash mixer, the wastewater will then flow by gravity through a
flow splitter box to two 25-foot diameter flocculator-clarifiers, where the
coagulated wastewater will be flocculated by gentle stirring in the floccula-
tion zone before being settled in the outer clarification zone.  The clarifier
effluent will then flow by gravity to the existing sewer leading to the muni-
cipal sewer system.  The clarifier sludge will be raked to the center wells
of the flocculator-clarifier units and pumped to sludge handling facilities to
be provided by ADM.

     The skimmings collected from the equalization basin and the flocculator-
clarifiers will be pumped separately using two positive displacement pumps
(P3, PS) to the acidulation facilities.   Separate handling and use of progres-
sive-cavity pumps are proposed to minimize plugging during winter months due
to the hardening of the skimmer oils.
           TABLE 10.  SUMMARY OF DESIGN BASIS AND MAJOR UNIT SIZES
General Design Basis                         Probability of Occurrence
                                                  50%5UI


Refinery Skimmer-Effluent:
   Flow, gpd                                   195,000     293,000
   COD, mg/1                                     4,000       6,400
   COD, Ib/day                                   6,500      12,000
   Population Equivalent                        38,000      70,000
   Fats, Oils, and Greases, mg/1                 1,550        *
   Fats, Oils, and Greases, Ib/day               2,500        *

Expected Treated Refinery Effluent:
   COD, mg/1                                     1,300       2,200
   COD, Ib/day                                   2,100       4,200
   Population Equivalent                        12,500      25,000
   Fats, Oils, and Greases, mg/1                   300        *
   Fats, Oils, and Greases, Ib/day                 500        *

Estimated Total West Plant Effluent:
   COD, mg/1                                       700       1,200
   COD, Ib/day                                   2,500       4,700
   Population Equivalent                        15,000      28,000
   Fats, Oils, and Greases, mg/1                   220        *
   Fats, Oils, and Greases, Ib/day                 740        *
                                       40

-------
           TABLE 10.  SUMMARY OF DESIGN BASIS AND MAJOR UNIT  SIZES
          	(Continued)	
General  Design Basis
   Probability of Occurrence
        50%90%
Estimated Sludge Production:
   Ib/day
   Percent Solids
   gal/day

Chemical Consumption:
   Lime, Ib/day
         gal/day at 10%
   Fed3, Ib/day
          gal/day at 40%
       1,350       2,000
           1.5         1.5
      11,000*      16,000*
         725       1,100
         875       1,300
         160        240
         500        725
insufficient data available to calculate.
                TABLE 11.  SUMMARY OF MAJOR EQUIPMENT SIZES
          Item

Equalization Basin, T-j:
   Number
   Dimensions
   Capacity
   Detention Time
   Mixer, M-l
   Materials of Construction
Effluent Pumps  (Pi, P2)
   Number
   Type
   Capacity
   Control

Skimmings Holding Tank
   Number
   Capacity
       Amount
One
50' X 50'  X 18'  deep (161  SWD)
300,000 gal (40,000 cu ft)
24 hours at 90% probable flow
One 15-HP platform-mounted
(Existing lagoon will  be modified
   sheet pile, side walls, and
   concrete lined bottom
Two (one alternating standby)
Non-clog, centrifugal
250 gpm at required TDK
Manual, liquid-level override
One
1000 gal
                                     41

-------
         TABLE 11.  SUMMARY OF MAJOR EQUIPMENT SIZES (Continued)
         Item

Skimmings Pump (Pa):
   Number
   Capacity
   Type

   Control
  (T2,
Flocculator-Clarifiers
   Number
   Required Flocculation Zone
      Detention Time
   Dimensions
   Design Overflow Rate for
      Settling Zone
   Detention Time in
      Clarifier Zone
   Overall Dimensions
   Volume of Each Unit
   Material of Construction
   Sludge and Scum Collection
Sludge Pumps (P4,
   Number
   Type

   Capacity
   Control
Skimmings Pump
   Number
   Type
   Capacity
   Control

Lime Feed Facilities
   Lime Storage Bin:
      Number
      Capacity
(T6):
                         Amount
                    One
                    50 gpm
                    Positive-displacement,
                       progressive  cavity
                    Liquid-level  in skimmings  tank
                     Two
                     20 minutes  at  90% probable
                       flow
                     8' diameter X  6'  height

                     500  gal  per sq ft per  day
                     5 1/2  hours at 90% probable
                       flow
                     25'  diameter X 14'  deep
                        (includes 2'  freeboard plus
                         2' sludge  zone)
                     6,900  cu ft or 51,500  gal
                     Steel
                     Units  provided with surface  skimmer.
                     sludge raked to center well
                     Two  (one  alternating standby)
                     Positive-displacement,
                       progressive-cavity
                     50 gpm at required TDH
                     Time controlled,  constant
                       speed
                     One
                     Positive-displacement,
                        progressive-cavity
                     50 gpm at required TDH
                     Liquid-level  in skimmings  tank
                     One
                     30 tons of hydrated lime,  or 75
                        days at normal feed rate
                                     42

-------
         TABLE 11.   SUMMARY OF MAJOR EQUIPMENT  SIZES  (Continued)
         Item

      Volume
      Material  of Construction
      Material  Stored

   Lime feeder:
      Number
      Capacity
      Type

   Mixing Tank  (Ty):
      Number
      Volume
      Dimensions
      Volume of Each Unit
      Material  of Construction
      Sludge and Scum Collection
   Sludge Pumps (P4, PS):
      Number
      Type

      Capacity
      Control

   Skimmings Pump (PS):
      Number
      Type
      Capacity
      Control

Lime Feed Facilities
   Lime Storage Bin:
      Number
      Capacity
      (T6):
      Volume
      Material
      Material

   Lime Feeder:
      Number
      Capacity
      Type
of Construction
Stored
                               Amount

                           1,500  cu  ft
                           Steel
                           Hydrated  lime
                           One
                           800 Ib  per  hour
                           Volumetric
                           One
                           1450 gal  or  190  cu ft
                           7'  diameter  X  7'depth  (5' SWD)
                           6,900 cu  ft  or 51,500  gal
                           Steel
                           Units provided with  surface
                              skimmer,  sludge raked to center
                              well
                           Two (one alternating  standby)
                           Positive-displacement,
                              progressive-cavity
                           50 gpm at required TDH
                           Time controlled,  constant  speed
                           One
                           Positive-displacement
                              progressive-cavity
                           50 gpm at required TDH
                           Liquid-level  in skimmings  tank
One
30 tons of hydrated lime,  or 75
   days at normal  feed rate
1,500 cu ft
Steel
Hydrated lime
                           One
                           800 Ib per hour
                           Volumetric
                                     43

-------
         TABLE  11.   SUMMARY OF MAJOR  EQUIPMENT SIZES  (Continued)
        Item

   Mixing Tank (T;):
      Number
      Volume
      Dimensions
      Lime Slurry Concentration
      Mixer, M-2
      Material of Construction

   Lime Slurry Transfer Pumps  (Py,  PS):
      Number
      Type
      Capacity
      Control

   Lime Slurry Storage Tank (Tg):
      Volume
      Dimensions
      Storage Capacity

      Mixer, M-3
      Material of Construction

   Lime Slurry Feed Pumps (Pg,  PIQ):
      Number
      Type
      Capacity
      Control
Ferric Chloride Feed System:

   Storage Tank (Tg):
      Number
      Capacity

      Dimensions
      Material of Construction

      Material stored

   Ferric Chloride Feed Pumps:
      (hi. PIZ)
      Number
      Type
       Amount
  One
  1450 gal  or 190 cu ft
  7'  diameter X 7'  depth  (5'  SWD)
  10%
  One at 3  HP
  Steel
  Two (one alternating standby)
  Non-clog, centrifugal
  50 gpm at required TDH
  Manual
  3,500 gal  or 467 cu ft
  9'  diameter X 10'  deep (81  SWD)
  2,400 Ib of lime or 3 days  at
     normal  feed rate
  One at 2 HP
  Steel
  Two (one alternating standby)
  Non-clog centrifugal
  10 gpm at required TDH
  Flow rate from equalization
     basin effluent
One
10,000 gal or 1,430 cu ft or
   24 days at normal feed rate
14' diameter X 10'  deep
Steel tank with acid-resistant
   lining
40% ferric chloride solution
Two (one alternating standby)
Positive-displacement pump
                                     44

-------
         TABLE 11.  SUMMARY OF MAJOR EQUIPMENT SIZES (Continued)
        Item

      Capacity
      Control

      Material of Construction

   Emergency Storage Basin (T-jg)
      Number
      Dimensions
      Capacity
      Materials of Construction
   Emergency Pump (PIS):
      Number
      Type
      Capacity
      Control
       Amount

0-40 gph
Flow rate of equalization  basin
   effluent
Acid-resistant
One
50' X 30'  X 18'  deep (SWD)
180,000 gal
(Existing lagoon will  be modified)
sheet pile side walls, and  concrete
lined bottom
One
Non-clog, centrifugal
250 gpm
Manual, liquid-level  override
Cost Estimate for Ferric Chloride and Lime Treatment with Clarification

     Preliminary estimates of the construction and annual (fixed and operating)
costs for the proposed wastewater treatment facilities are shown in the
following tabulations.  The total construction cost included a construction
contingency, but excluding engineering design costs, is estimated to be
$393,000.  The total annual cost, including operating costs (labor, maintenance,
utilities, and chemicals) and fixed cost {depreciation, interest, insurance,
and taxes) is estimated to be $100,300.
                TABLE 12.  SUMMARY OF CONSTRUCTION COSTS*
                   Item

           Equalization Basin
           Flocculator-Clarifiers
           Lime Feed System
           Emergency Storage Basin
           Skimming Tanks
           Control and Chemical Building
          Amount

         $54,000
          95,000
          19,000
          32,000
           6,000
          40,000
                                     45

-------
          TABLE  12.  SUMMARY OF CONSTRUCTION COSTS*  (Continued)
                   Item                         Amount
              Subtotal                           258,000

           Piping (at 15$)                        37,000
           Electrical (at 10%)                    26,000
           Instrumentation  (at  6%)                16,000
           Site Work                               5,000

              Subtotal                           342,000

           Construction Contingency  (15%)         51,000

              Total  Construction  Costs           393,000
           *Based on 1969 construction prices.
              TABLE 13.  SUMMARY OF ANNUAL ESTIMATED COSTS1*
               Item                                  Amount
Operating Costs:
   Labor Cost at $5.00/hr, 8 hrs/day,  260 days/hr   $10,400

   Maintenance
      Mechanical                 at 7% of $ 65,000    4,500
      Structures                 at 2% of $168,000    3,400
      Electrical and Instruments at 7% of $ 42,000    2,900

   Chemicals:
      Lime, 135 tons/yr at $26.00/ton                  3,500
      Ferric Chloride, 30 tons/yr at $80.00/ton       2,400

   Utilities:
      Electrical at 0.015/KWH, 700 KW-hr/day          4,000

             Total Operating Costs                   31,100
                                   46

-------
              TABLE 13.  SUMMARY OF ANNUAL ESTIMATED  COSTS*
                         (Continued)
               Item                                  Amount
   Fixed Costs:
      Depreciation (18 years straight line)          22,000
      Interest (10%)                                 39,300
      Insurance and Taxes (2%)                        7,900

             Total Fixed Costs                       69,200

             Total Annual Costs                     100,300

*Costs are rounded to nearest $100, 1969 prices.
                                     47

-------
                              SECTION VIII

                 DESCRIPTION AND EVALUATION OF INSTALLED
                    WASTEWATER MANAGEMENT FACILITIES
     Process evaluation was done for the equipment in Decatur.   Figure 11
is a flow diagram for the treatment facilities.  Flows and concentration
are approximate and are based upon operating records.

FACILITIES AT DECATUR WEST PLANT

     It was decided by ADM to install one 186,000-gal clarifier at the
Decatur West Plant.  It was felt that this clarifier along with process
modifications described below would bring the waste strength to within
acceptable limits.  If this was unsuccessful, the process recommended by
the consultant could be installed incorporating this clarifier.  This was
successful, so the ferric chloride and lime flocculation system was not
installed.

1.  Condensate Recycle:  The condensate generated in the refinery, while
    not having any BOD, contributes a significant hydraulic load to the
    treatment facility.  Therefore, this water was recycled for use in
    refining and water wash.   Because of this, there was no net increase
    in hydraulic load as production increased resulting in longer residence
    time in the treatment facility.  Water recycled is approximately 50,000
    gallons per day.

2.  Soapstock Concentration:   It was found that far too much flush water was
    being used on the refining centrifuges.   This resulted in soapstock with
    moisture in the 80% to 90% range.  This caused the acidulation facili-
    ties to be overloaded and resulted in poor splitting due to inadequate
    reaction time.  By simple external  piping modifications, the soapstock
    moisture was decreased to 30% to 50%.  This gave a residence time suf-
    ficient to treat the soapstock and resulting acid liquor even after
    expansion.  The water eliminated from the waste stream was  at least
    50,000 gallons per day.

3.  Oil Spills and Malfunctions:  Projects were undertaken to eliminate
    possibilities of oil losses due to malfunctions.   All areas where the
    possibility of an oil spill existed were piped to the calcium chloride
    treatment system.  Each vacuum vessel which could overflow to the baro-
    metric cooling tower via the ejector system was equipped with high level
    alarms.
                                      48

-------
-£»
ID
CaCI2 FLOOR
J 1
SOAPSTOCK 5500
WA9HWATFFT TAMI/ ^u»u*
WHwrivYMi trt TANK
H2S04
ACIDULATION
*
ACIDULATION
25,000 GAL/DX
^ CONCE
(SALE
42,000 PPD
DRY BASIS
RAW SOAPSTOCK
STORAGE
RAW SOAPSTOCK
HHAIN- SLOWDOWN GREASY WATER
uimiNv, 0-30,000 GPD COOLING TOWER
0-1000
R
DO GPD i
NaOH
i ,
NEUTRALIZATION
1 ' \ I, i . C
PROCESS
*Y WASTEWATER
:NTRATED SOAPSTOCK
:ABLE BY-PRODUCT)
I40O PPD
FLOATING MATERIAL]
(SKIMMINGS)
TO SOAPSTOCK
STORAGE
PPD * *
*T DEODORIZER

MUNICIPAL WATER
ZEOLITE SOFTENING
(MAKEUP WATER)

•JBOILER


^ CLEAR WATER
COOLING TOWER

v (HOLDING LAGOON L
^ 	 ^^n V/I»L/I t»\j • L.Mwwi'i p

L MECHANICAL
^* SKIMMING TANK
1 \

(SANITARY WASTE
TO
DECATUR MUNICIPAL -—
SEWERAGE SYSTEM
SOLVENT
EXTRACTION
WASTEWATER

150,000 GPD
450 PPD BOD
ZEOLITE
REGENERATION
SLOWDOWN
SLOWDOWN to

7000 COD
-In ARIF1FR M.
-|v/L.Mr{ir lt.rl ^
J 150.000 GPD
_ 1 2O6 -500 FAT
500-1000 COD




AUTOMATIC SAMPLER
"AND FLOW METER

       FROM CAUSTIC REFINING
                   Figure  11.  Decatur wastewater treatment facility.

-------
     It has been difficult to obtain meaningful  operational  data  on  the
clarifier for several  reasons.   The refinery started  refining  corn oil
weekly at approximately the same time the clarifier was put  into  operation.
It was found that the wastewater generated by this process was more  difficult
to treat than that generated by soybean oil.

     The clarifier offset the high sewer load generated by the refining  of
corn oil.  Therefore, it is difficult to make a meaningful before and after
comparison in terms of overall load.  Reduction in COD will  be given for
a particular treatment step in terms of before and after treatment,  as well
as a net per pound processed reduction in strength after the clarifier was
installed.

     Waste treatment facilities consist of chemical flocculation  equipment,
a 30,000 gal skimmer, a 150,000 gal holding lagoon and a clarifier.   Figure
12 is a plot plan of the existing treatment area at Decatur.

     The calcium chloride treatment system is described in  Section  VI.
All refinery wastewater and floor washings are treated in this system.  As
can be seen from Table 3 of Section VI, this system reduces  the  COD by
approximately 92%.

     Table 14 presents Ib BODs and Ib fat per pound oil processed data from
April 1969 to June 1974.  The calcium chloride treatment was started in
October 1969.  This data is presented in Figures 13 and 14 with significant
elements of the treatment research and installation noted.   Fat analysis
was not done by the city before 1970.  BOD5 and fat analysis for October,
November, and December 1970 were not available.

     The refinery was down due to a fire November 1969, and  expanded pro-
duction resumed April 1970.

     Table 15 presents population equivalents, oil processed and Ib 8005
and fat per pound of oil processed for the six month period  before the cal-
cium chloride treatment was installed and the six month period after the
expanded refinery was started.  There was a net reduction of 71 % of the
6005.  No fat tests were run before the calcium chloride treatment was started
because the City of Decatur did not require them at that time.  The last
part of Table 13 is for 1973 after the clarifier was installed and all pro-
cess modifications were made.  BODs and fat reductions for each process
are summarized as follows:

Before Treatment:
      .0135 Ib BOD per  Ib OIL processed
      .0041 Ib FAT per  Ib OIL processed, estimated

After Calcium Chloride Treatment:
      .0039 Ib BOD per  Ib OIL processed
      .00099  Ib FAT per Ib OIL Processed

      71% reduction in  BOD


                                       50

-------
                                             TO DSD
       TRUCK
      LOAD-OUT
SKIMMER
    TANK'
TO SOAPSTOCK

r~
i


%-£'
PUMP
\
\
\
   HOUSE
JPUMP HOUSE
[OVERFLOW
                                 \
                                   \
      SKNMME
                      CLARIFIER SUMP
I  SOAPSTOCK
2 RECOVERED  OIL
3 COOKER
4 NEUTRALIZING
5 SULFURIC  ACID
6 CAUSTIC


 SKIMMER
 BYPASS VALVE

GREASY WATER
 OVERFLOW
                                                                          OVERFLOW
                                                                          SKIMMER BYPASS
                                                                          TO CLARIFIER
                   SETTLING  BASIN
                                                                                    TANK
                                10  SANITARY
                                LINE TO CITY
                           Figure 12,  West plant treatment flow diagram.

-------
Ol
ro
           z.o
        CD
        O
        O
03

O


x  1.0

o
                                CaCI2  TREATMENT INSTALLED
                                                                         STUDY COMPLETED
CLARIFIER  STARTED
CORN  OIL  REFINING  STARTED
ELECTROYSIS  SYSTEM ABANDONED
                                                                 TREATMENT COMPLETED
                   1969     I   1970     I    1971     I    1972     I    1973     I   1974
                                   Figure 13. Pounds BOD per pound oil processed.

-------
OJ
       CD


       3
       •>.
       r
       CD

       O
TJ
TO
O
O
m
CO
0)
m
o
       O
        01
           2.0
           1.0
                                 IL
  n
11
                                                 T
                                                       l

                        JlJ1!
                   1969   I    1970   '    J97l   '    1972   '   1973   '    1974

                                               MONTH
                            Figure 14.  Pounds fat per pound oil processed.

-------
After Total Treatment System:
     .0019 Ib BOD per Ib OIL processed
     .00050 Ib FAT per Ib OIL processed

     5155 reduction in BOD over primary
         chemical treatment
     50% reduction in FAT over primary
         chemical treatment

     86% overall  BOD reduction
     86% probable FAT reduction
         = .0036 Ib per Ib processed

     The clarifiers and system modifications resulted in a further reduc-
tion of 50% of the BODs and fat per pound processed.   The overall  reduction
in BODs was 86%.   This is probably close to the overall  fat reduction
for the system based on the overall reduction in the  second step.

     From the primary chemical treatment, the calcium chloride treatment
effluent gravity flows to a sump where it is mixed with  barometric con-
denser cooling tower overflow and surface water from  the acidulation area
and pumped to the skimmer.  The skimmer has a volume  of  30,000 gal and is
diagrammed in Figure A-2 of Appendix A.  The skimmer  retains any oil spilled
in acidulation and some additional  floe from the calcium chloride treatment
system.  All skimmings go to acidulation.
                TABLE 14.   WEST PLANT EFFLUENT ANALYSIS*
                Oil                                 Ib BOD/      Ib FAT/
             Production,       BOD,      Fat,       Ib Oil        Ib Oil
Month          1b/day         Ib/day    Ib/day     Processed    Processed

Apr. 1969     407,000          6,331      ~         .0155
May           407,000          8,186      ~         .0201
Jun.          407,000          3,281      —         .0081
Jul.          409,000          8,874      «         .0217
Aug.          348,000          4,845      —         .0139
Sep.          490,000          4,420     —         .0090
Oct..         339,000          2,159      ~         .0063
NOV.:;
Dec.

Jan. 1970
Feb.
Mar.
Apr.          603,000          2,040      893        .0034        .00150
May           726,000          3,417      448        .0047        .00062

-------
TABLE 14.  WEST PLANT EFFLUENT ANALYSIS* (Continued)


Month
Jun.
Jul.
Aug.
Sep.
Oct.
Nov.
Dec.
Jan. 1971
Feb.
Mar.
Apr.
May
»»-^
Jun.
Jul.
Aug.
Sep.
r
Oct.
Nov.
Dec.
Jan. 1972
Feb.
Mar.
Apr.
May
•w^
Jun.
Jul.
Aug.
Sep.
w ff m
Oct.
Nov.
Dec.
Jan. 1973
Feb.
Mar.
Apr.
May
i iv* jr
Jun.
W M 1 1 •
Jul .
Aug.
Oil
Production,
Ib/day
803,000
852,000
829,000
660,000
1,043,000
712,000
788,000
895,000
963,000
845,000
930,000
1,130,000
915,000
1,101,000
1,208,000
792,000
801,000
696,000
868,000
1,020,000
958,000
1,118,000
920,000
1,107,000
872,000
753,000
635,000
854,000
705,000
1,262,000
1,046,000
742,000
1,021,000
987,000
1,047,000
861,000
980,000
835,000
729,000

BOD,
Ib/day
2,703
3,026
3,536
2,567
—
—
--
1,480
1,534
1,640
4,450
2,470
1,480
1,596
1,994
5,142
3,900
2,926
3,593
3,450
2,188
2,688
3,117
2,156
2,338
2,034
1,414
1,921
1,089
892
764
1,836
1,156
1,887
3,757
1,683
952
1,156
1,1224

Fat,
Ib/day
587
599
1,066
722
-
—
--
460
650
699
2,479
633
427
600
741
2,157
785
590
1,124
1,149
375
557
1,523
402
818
652
807
864
303
330
226
241
139
472
517
568
183
430
228
Ib BOD/
Ib Oil
Processed
.0034
.0035
.0043
.0039
--
—
"•—
.00165
.00159
.00194
.00478
.00219
.00162
.00145
.00165
. 00649
.00487
.00420
.00414
.00338
.00228
.00240
.00339
.00195
.00268
.00270
.00223
.00225
.00154
.00071
.00073
.00250
.00110
.00190
.00360
.00190
.00100
.00140
.00170
Ib FAT/
Ib Oil
Processed
.00073
.00070
.00128
.00109
— —
--
•• ~
.000514
.000675
. 000827
.002660
.000560
. 000466
.000545
.000613
.002723
.000980
.00084
.001295
.001130
.000390
.000498
.001650
.000363
.000938
.000866
.001270
.001011
.000430
.000261
.000216
.000320
.000140
.000480
.000490
.000660
.000190
.000520
.000310
                         55

-------
          TABLE 14.  WEST PLANT EFFLUENT ANALYSIS* (Continued)



Month
Sept.
Oct.
Nov.
Dec.
Jan. 1974
Feb.
Mar.
Apr.
May
Jim.
Oil
Production,
Ib/day
733,000
942,000
900,000
1,048,000
1,030,000
1,294,000
1,089,000
1,074,000
1,167,000
1,363,000

BOD,
Ib/day
935
1,700
1,632
2,856
1,525
2,535
1,904
2,740
2,671
3,420

Fat,
Ib/day
424
559
496
1,217
437
820
529
730
645
786
Ib BOD/
Ib Oil
Processed
.00130
.00180
.00180
.00270
.00148
.00196
.00175
.00255
.00229
.00251
Ib FAT/
Ib Oil
Processed
.000580
. 000590
.000550
.001160
.00420
.000630
.000490
.000680
.000550
.000580
*Total effluent approximately 300,000 to 400,000 6PD through grant  period.
+Down for refinery fire.
  TABLE 15.  DECATUR WEST PLANT BOD5 AND FAT PER POUND OF OIL PROCESSED



Month
Apr. 1969
May
Jun.
Jul.
Aug.
Sep.
Oct.
Nov.
Dec.

Avg. Popula-
tion Equiv.
37,200
48,100
19,300
52,200
28,500
26,000
12,700
3,100
8,400

FAT, BOD,
Ib/day Ib/day
6,331
8,186
3,281
8,874
4,845
4,420
2,159


Oil Produc-
tion/day,
Ib
407,000
407,000
407,000
409,000
348,000
490,000
339,000



Ib BOD/
Ib Oil
.0155
.0201
.0081
.0217
.0139
.0090
.0063



Ib FAT/
Ib Oil









                   Calcium chloride treatment started
Jan. 1970
Feb.
Mar.
              5,800
              6,600
             13,900
                                     56

-------
  TABLE 15.   DECATUR WEST PLANT BOD5  AND  FAT  PER  POUND OF OIL PROCESSED
             (Continued)
                   Calcium chloride treatment started



Month
Apr.
May
Jim.
Jul.
Aug.
Sep.

Avg. Popula-
tion Equiv.
12,000
20,100
15,900
17,800
20,800
15,100

FAT,
Ib/day
893
448
587
599
1,066
722

BOD,
Ib/day
2,040
3,417
2,703
3,026
3,536
2,567
Oil Produc-
tion/day,
Ib
603,000
726,000
803,000
852,000
829,000
660,000

Ib BOD/
Ib Oil
.0034
.0047
.0034
.0035
.0043
.0039

Ib FAT/
Ib Oil
.00150
.00062
.00073
.00070
.00128
.00109
                        Total  system in operation
Jan. 1973
Feb.
Mar.
Apr.
May
Jun.
Jul.
Aug.
Sep.
Oct.
Nov.
Dec.
10,800
6,800
11,100
22,100
9,900
5,600
6,800
7,200
5,500
10,000
9,600
16,800
241
139
472
517
568
183
430
228
424
559
496
1,217
1,836
1,156
1,887
3,757
1,683
952
1,156
1,224
935
1,700
1,632
2,856
742,000
1,021,000
987,000
1,047,000
861,000
980,000
835,000
729,000
733,000
942,000
900,000
1,048,000
.0025
.0011
.0019
.0036
.0019
.0010
.0014
.0017
.0013
.0018
.0018
.0027
.00032
.00014
.00048
. 00049
.00066
.00019
.00052
. 00031
.00058
.00059
.00055
.00116
     The overflow from the skimmer gravity flows to a sump where it  is
pumped to the clarifier.  The clarifier is a 183,500 gal  Rex Wastewater
Clarifier (Figure C-l of Appendix C).  The clarifier is 50 ft in diameter
with a surface area of 1950 sq ft.  This provides an overflow rate of
75 gal per sq ft per day based on a flow of 150,000 gal per day.  A  60 day
average of clarifier influent versus clarifier effluent COD's resulted in
an average reduction of 45% through the clarifier.  Samples were based on
24 hour composites but were not flow proportioned.  This  data is presented
in Table 16.
                                    57

-------
TABLE 16.
CLARIFIER
COD REDUCTION


Date
11/08/71
11/09/71
11/10/71
11/11/71
11/12/71
11/15/71
11/16/71
11/17/71
11/18/71
11/19/71
11/22/71
11/23/71
11/24/71
11/26/71
11/29/71
11/30/71
12/01/71
12/02/71
12/03/71
12/06/71
12/07/71
12/08/71
12/09/71
12/13/71
12/14/71
12/15/71
12/16/71
12/17/71
12/20/71
12/21/71
12/22/71
12/27/71
12/28/71
12/29/71
12/30/71
1/03/72
1/04/72
1/05/72
1/06/72
1/10/72
1/12/72
1/13/72
1/14/72
Influent
COD (mg/1)
1369
790
3579
1790
2900
1970
3080
2100
1840
2250
1840
2260
9731
3550
1210
5030
10000+
4460
3760
2780
2160
8760
6000
2580
1540
4740
1800
5665
1950
825
3500
2407
2064
3326
8750
1080
2455
10000+
2170
2275
3375
1725
3560
Ef f 1 uent
COD (mg/1)
1316+
790
1555
1420
1050
579
1100
526
684
420
920
893
2314
1210
1210.,
2680?
5360
2310
1900
1700
1440
4950§
1560
2580
2830
2260
1800
3141#
1900
2000
1250
1700
1746
1267^
3168#
585
1820
2300
1171
1455
2250
1725
3000
58

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             TABLE 16.   CLARIFIER COD REDUCTION  (Continued}
                               Influent              Effluent
             Date             COD (mg/1)             COD  (mg/1)

            1/18/72              1595                 1740
            1/19/72              2465                 2247
            1/20/72              1885                   725
            1/21/72              1667                   943
            1/24/72              1392                   956#
            1/26/72              2375                 1241
            1/31/72              1692                 1692
            2/01/72              1690                 1400
            2/02/72              2000                   693
            2/03/72              1181                 1155
            2/07/72               970                   908
            2/08/72              1196                   700
            2/09/72              1847                   960
            2/10/72              2000                   763
            2/11/72              1456                   640
            2/14/72              2408                 2254

            MEAN                 2997                 1642

*Reduction in COD is 45%.
+Acid liquor to lagoon.
^Overflow soap-stock tank.
iAcid liquor to clarifier-black
#Corn oi1.

     Clarifier influent and effluent was  monitored for 20 consecutive days
from March 24 to April 14, 1972, and analyzed for fat, COD, pH, and tempera-
ture.  This data is presented in Table 17 and Figures 15, 16,  17, and 18.
Samples were taken on a 24 hour composite, but were not  flow proportioned,
A reduction in fat of 53% and a reduction in COD of 41%  was noted.

     The temperature of the effluent was  stabilized at 34°C.   The pH was
slightly decreased throughout the period.  The pH of the influent was high
April 9 through April 11 due to a leaking seal on a caustic pump.  The clari-
fier kept the pH below 9.5 throughout this period and returned to normal quickly
after the seal was repaired.

     High waste strength when the plant was on corn oil  was primarily because
corn oil was not degummed before refining.  This was because no appreciable
market for corn lecithin existed.  Water  soluble phosphatides  are separated
with the soapstock and some come out in the wash-water.   Their gums are not
readily precipitated by calcium chloride  and a high wasteload  results.

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12

II

10

 9

 8

 7

 6

 5

 4

 3
                            BROKEN  CAUSTIC LINE
 --INFLUENT
— EFFLUENT
      I   I    I   I   I   I    I   I   I   I    1   I   I   I    I   I   I    I   I   I   I
  24 25 26  27 28 29 30  31
I   2  3  4   5  6  7   8   9  10 II  12  13  14

    DAY MARCH-APRIL   1972
                        Figure  15.  Clarifier pH vs  day ADM Decatur.

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60
50

1 40
m
m 30
0
20
10
n
- A A /
	 ,-' • ,'--.y \

• s
i
—
\
\
" — J 1 x — — • — -^
l^x'
.-.--- IMPI IIPMT
" *~ ~ inrL.ucni
•*•.«»•
	 F FFLU E NT
1 I 1 1 1 1 1 1 1 1 1 i 1 1 1 1 1 1 1 1 1
24 25  26 27  28 29 30  31   I   23   4  5   6  7  8   9  10 II  12  13  14
                        DAY  MARCH-APRIL 1972

       Figure 16.  Temperature vs day ADM clarifier, Decatur, Illinois.

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ov
          5000
       o
       o
          4000
          3000
          2000
          1000
                                  INFLUENT


                                  EFFLUENT
                                                            j CORN |
                              \	
1   I   L   I   L  I
                                        1 J_ J_  I   I    I   I   I   I   I    I   I   I   I
              24 25  26  27 28 29 30 31  I  2   345  6  78  9  10  II  12  13  14
                                         DAY  MARCH-APRIL 1972
                              Figure 17.  Clarifier COD vs day ADM Decatur.

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                              INFLUENT

                              EFFLUENT
                                 CO-CORN OIL PROCESSING

                                 SO * SOYBEAN OIL  PROCESSING
CO
1800


1600


1400


1200


1000


 800


 600


 400


 200
                       I   I   I   I   I   I   I   I   I   I   I    I
I
I
I
I
I
I
I
1
                                                                   I   I
                  24  25  26 27 28 29 30 31  I   2  3  4  5  6  7  8   9   10  II  12  13  14


                                     DAY MARCH-APRIL  1972

                            Figure 18.  Fat vs day Decatur ADM clarifier.

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Gums in the soapstock are not converted to fatty acids  and remain  in  the  acid
water phase.  This was and has remained a problem.   However,  since 1972
a small market for corn lecithin has been cultivated by sales,  which  has
partially resolved the problem.

     The COD of the acid liquor is  highly variable  depending  on the nature
of the soaps and the amount of floor washings  in a  particular batch.   Therefore,
the lagoon influent COD's give only a range of values that can  be  expected
at a given time.  The volume of acid liquor is approximately  25,000 gal
per day produced in three or four equal batches. The steady  increase in
strength of the effluent indicates-a need to clean  the  lagoon periodically,
every two or three months.  (Table  18)

Economic Analysis of Decatur West Refinery Waste Treatment System

     From the process evaluation, it will be assumed fat losses were  reduced
.0036 Ib per pound processed by the calcium chloride and clarification sys-
tem.  This is recovered as acid oil, the price of which is highly  variable.
This is an average of 3089 Ib per day based on a daily production  of  858,000
Ib of oil.  Table 19 is the total installation and  operation  cost  of  the  cal-
cium chloride treatment system and  the clarifier.  Tables 20  and 21 are
a summary of waste treatment costs  on a per Ib 8005, per Ib fat removed,  per
gal treated, and treatment cost per kg oil processed.  The oil  recovered  must
be processed by acidulation at a cost of 2
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           TABLE 17.  DECATUR CLARIFIER OPERATION*  (Continued)
  Date    pH      Fat      COD    Temp.       pH      Fat      COD     Temp.
                (mg/1)   (mg/1)    (C°)             (mg/1)    (mg/1)     (C°)
4/08/72
4/09/72
4/10/72
4/11/72
4/12/72
4/13/72
4/14/72

Average
 6,
10.
10,
10.
 6.
 7,
 6,
1216
 244
 253
  47
2136
 613
 682

 544
3416
 627
 454
 247
2757
1421
2375

1388
44
44
53
6.1
5.8
7.6
9.4
6.8
6.4
5.9
270
133
 66
 18
 87
118
191

223
960
808
250
418
467
433
773

818
34
33
34
*Reduction is 59% for fat and 41% for COD.
                 TABLE 18.  LAGOON OPERATION COD (mg/1)1
              Date

            1/05/72
            1/15/72
            2/07/72
            2/22/72
            2/28/72
            3/06/72

            Average
                      Influent

                       14,600
                        8,650
                       11,475
                        7,618
                       19,260
                       14,250

                       12,642
                                  Effluent

                                    3,580
                                    5,600
                                    6,235
                                    7,194
                                    9,250
                                   10,000

                                    6,976
*COD removal is 45%.
                                    65

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TABLE 19.  INSTALLATION AND OPERATION COSTS FOR WEST REFINERY  WASTE  TREAT-
           MENT SYSTEM
                Item                                  Cost per year

Calcium Chloride (Costs for 1969):
   Depreciation @ 10% per year based on total
     capitalized cost of $25,000                       $  2,500
   Calcium Chloride @ 7i per Ib dosage of 0.25%          21,308
   Maintenance                                            1,000
   Labor 4 hours per day                                  7,500
                                                       $ 32,308

Clarifier (Costs for 1971):
   Depreciation @ 5.5% per year based on total
     capitalized cost of $96,621                        $  5,367
   Utilities                                              5,000
   Interest                                               9,662
   Insurance and Taxes                                    1,932
   Maintenance
     Mechanical 5%                                        5,000
     Structures                                           1,000
   Labor 1 man                                           15,000
                                                       $ 42,961

Total Treatment Cost                                   $ 75,269
                   TABLE 20.   SUMMARY OF TREATMENT COSTS
       Item                           Treatment     Clarifier      Total
Cost per day                            $  88          $118        $206
BOD removal (Ib per day)                8236          1716        9952
Cost £ per Ib BOD removed               1.06          6.87        2.07
Fat removal (Ib per day)                2660           420        3080
Cost i per Ib fat removed               3.3          28.1          6.7
Cost i per gal                          .059          .077        .136
   (based on 150,000 gal per day)
Cost t per kg oil produced              .019          .026        .045
                                   66

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                TABLE 21.   NET COSTS (COST MINUS REVENUES*)

Acid Oil
Price
4* per Ib
18* per Ib
Cost per
1000 liters
$.251
-$.510
Cost per
1000 gal
$0.95
-$1.93
Cost per
kg Oil Processed
.032*
-.063*
Revenue:  4* per Ib Acid Oil   Revenue = (.04-.02)  (3080)  =  $61.76 per day;
         18* per Ib Acid Oil   Revenue = (.18-.02)  (3080)  = $494.08 per day.
                                    67

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          HA
-INLET
MD RAIL
 50' *

DRIVE  UNIT,
                                                           RRIDGE
T3
T3
n>


ex
-J.

X


3>
          SKIMMER




     ^SCUM BAFFLE
                                     u
                                                           WEIR

                                                        WELL
                                                       EFFLUENT
                                                        TROUGH
                                                               SWEEP ARMS
                                         TORQUE

                                           TUBE
                                                                        -a  rn
                                                                        -o  o
                                               n  i—i
                                               oo  x
                                                                     STEEL TANK'
                 Figure A-1.  Rex wastewater clarifier (186,500 gallons).

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VO
         7'-6"

                      /
                  OIL  DISCHARGE
                   O
INLET
                                                   ^57-6"
                                          Figure A-2.  Walker skimmer.

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APPENDIX B.   ANALYTICAL PROCEDURES

Fats. Oils,  and Greases - Analytical  Procedure Used During  R.F.W.  Survey

1.  The samples were thoroughly shaken (and heated, if necessary)  and
    were acidified with 5 ml  of concentrated h^SCty and heated on a steam
    bath for 15 to 30 minutes.

2.  The samples were cooled and 50 ml  of hexane added to the sample bottle
    (100 mg  of hexane was added if an  overabundance of grease was  present).

3.  The sample bottle was shaken manually for 30 seconds at about  240
    shakes per minute rate.

4.  The entire contents of the bottle  were poured into a one-liter separatory
    funnel and allowed to separate.  The water layer was decanted  into
    a one-liter graduated cylinder and the volume recorded.  The hexane was
    then allowed to filter through a filter-eel precoated,  whatman No.  1
    covered, buchner funnel.   The precoat consisted of about 30 ml of a
    10 gm/1  slurry of filter-eel.

5.  The sample bottle, transfer funnel,  and separatory funnel were rinsed
    with about 10 - 15 ml of hexane and  this was added to the 50 ml and also
    filtered.

6.  The filtered hexane was collected  in test tubes in the  vacuum  flasks
    and transferred to 30-ml  capacity, pre-tared aluminum weighing dishes
    and evaporated on a steam hot plate.  Any water-hexane  emulsion was
    also filtered and evaporated.

7.  The evaporated dishes were placed  in a 103°C oven for at least one
    hour, transferred to a desicator and re-weighed.

8.  Fats, oils, and greases,  mg/1 =

    Final Weight - Initial Weight of  Dish
       in mg	in mg	x 1000
                  ml sample
                                      70

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A-D-M COD Test Procedure

1.  Prepare sample of aliquot and place in 250 ml  reflux flask.   (Size
    of sample depends on strength of aliquot - 10  ml  if COD  is  1000
    below or proportionately less if COD is higher.)

2.  Add 10 ml potassium dichromate (0.125 n), 15 ml cone,  sulfuric acid
    and pumice to each flask and reflux for 15 minutes.

3.  Set control and titrate with ferrous ammonium  sulfate (0.067  n)  to
    determine normality  .125   (10 ml  potassium dichromate,  15 ml
                        ml  used                           ,
    cone, sulfuric acid, cool to 60°C,  add 3 drops ferroin ,  50 ml
    distilled water and titrate).

4.  After 15 minutes cool flask to below 60°C and  titrate with  ferrous
    ammonium sulfate (0.067 n) recording ml used.

5.  Calculate COD = A-B x normality x 8000
                          ml of sample

    A = ml of titrant for control
    B = ml of titrant for sample

    Normality =     1.125
                ml of control


 Ferroin Indicator = 1.485 grams 1.10 Phenanthroline  and 0.695  grams
 Ferrous Sulfate per 100 ml distilled water.
                                  71

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APPENDIX C.  WASTE TREATMENT FACILITIES AT ADM,  LINCOLN,  NEBRASKA

     The calcium chloride treatment is essentially the same as  that  in
Decatur and will not be discussed here.

     All refinery effluent is pumped to a 30,000 gal  split box  where it  is
skimmed and overflows to a series of sumps where it is mixed with blowdown
from the barometric condenser cooling tower and  pumped to the skimmer.
The skimmer effluent is pumped to the clarifier.  The water from the clari-
fier flows through the sampling station to the sanitary sewer.   (Figure  C-l)

     The water from acidulation is also pumped to the split box.   The clari-
fier water is always dark in color due to the acid liquor; however,  the  clari-
fier does an effective job of BOD§ removal.   Acidulation, a major contributor
to the sewer load, was shut down in May 1971  and started again  in September
when the clarifier was put into operation.  A drop in the sewer load was noted
when acidulation was shut down and no increase was noted when it was started
again with the clarifier in operation.  Refer to Figures C-2, C-3, C-4,  and
Table C-l.  Therefore, a before and after comparison  was made for the period
after the clarifier was started and before acidulation was shut down.
           TABLE C-l.  ANALYSIS OF DISCHARGE TO MUNICIPAL SEWER


Month
Jan. 1971
Feb.
Mar.
Apr.
May
Jun.
Jul.
Aug.
Sep.
Oct.
Nov.
Dec.
Jan.- 1972
Feb.
Mar.
COD
Ob/day)
3191
4128
4467
4116
1589
1182
1590
1907
1497
1589
1510
1472
1765
1118
662
Suspended
Solids (mg/1)
756
982
780
735
272
256
248
309
209
225
183
155
145
199
97
Fat
(mg/1)
310
571
508
484
233
206
229
246
213
229
181
160
5150
99
73
                                     72

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CO
             CdCI2   FLOOR DRAINS
                                       BLOWDOWN
                                       0- 30.000 GPD
                                       0-1000 PPM
                                            FAT
                                   GREASY'WATER
                                   COOLING TOWER
                                    DEODORIZER
                                               JL
                    J
                           SOLVENT
                          EXTRACTION
                          WASTEWATER
         PERIODIC SK
         SOAPSTOCK <
TO
           H2S04
                 ~L
          ACIDULATION
                               25,000
                                GPD
                                       NaOH
              NEUTRALIZATION
                ACIDULATtON PROCESS
       7000 PPD  '
       DRY
       BASIS
                      WASTEWATER

                    ^CONCENTRATED SOAPSTOCK
                      (SALEABLE  BY-PRODUCT)
                                                 MUNICIPAL WATER
                               ZEOLITE  SOFTENING
                                 MAKEUP WATER
                          ZEOLITE
                                 -HBOIL.ERI-
                     REGENERATION
                       BLOWDOWN
                                                   CLEAR WATER
                                                  COOLING TOWER
                                                    BLOWDOWN
                                  MECHANICAL
                                SKIMMING TANK
                    -JCLARIFIER
                         ^
30,000 PPD
DRY BASIS
                              1500 PPD
            RAW SOAPSTOCK
               STORAGE
      RAW SOAPSTOCK
          [^FLOATING MATERIAL i
           (SKIMMINGS)
          TO SOAPSTOCK
          STORAGE
     SANITARY WASTES!
        TO
LINCOLN  MUNICIPAL
  SEWERAGE SYSTEM""
                                        AUTOMATIC SAMPLER
                                        AND FLOW METER
      FROM CAUSTIC REFINING
                         Figure C-l.  Lincoln wastewater treatment facility.

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     These data are presented in Figures  C-2,  C-3,  and  C-4.   A  comparison
of parameters for January - April,  1971 with October  1971  -  March  1972
gives the following average reductions:
                     Parameter

                        Fat
                        SS
                        COD
% Reduction

    66.3
    78.7
    65.6
     The higher reduction in suspended solids was expected,  since this
type of material is treated especially well  by the clarifier.

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Ul
              500
              400
              300
              200
               100
                                         ACIDULATION    CLARIFIER  STARTED
                      I	I	I    I    I    I    I    i    I    I    I    I    I    I    I
                      J   FMAMJJASONDJ   FM
                            MONTH   JANUARY-1971 THRU  MARCH" 1972
            Figure C-2.  ADM Lincoln, Nebraska average mg/1  fat vs month January 1971-March  1972.

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CO
c
m

o
m
o
CO

O
o
CO
1000



 900



 800



 700



 600



 500



 400



 300



 200



 100



   0
ACIDULATION  ICLARIFIER  STARTED
                I	i   I    I    I    I    I    1
                    1   I    I    1    1
                       MAMJJASONDJ



                        MONTH  JANUARY-1971  THRU MARCH-1972
                                                                M
         Figure C-3.  ADM Lincoln, Nebraska suspended solids vs month January 1971-March 1972.

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o
o
a
o
5
o
z
m
zo
m
     5000
     4000
3000
     2000
      1000
^ACIDULATION

DOWN
CLARIFIER
rSTARTED
1 1 1
J F M
| |
A N
1 1 1 1 1 1 1 I 1 1
AJJASONDJFM
                            MONTH JANUARY-1971  THRU MARCH-1972


       Figure C-4.  ADM Lincoln, Nebraska average Ib OOD/day vs month January 1971-March 1972.

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                                  SECTION X

                                BIBLIOGRAPHY
Bailey, A. E.  Industrial Oil and Fat Products, New York, Interscience
Publishers, Inc.  1945.

Standard Methods for the Examination of Water and Wastewater, 12th Edition.
New York, American Public Health Association.1965.

Weston, R. F.  "Conceptual Design Report, Upgrading of West Plant Wastewater
Treatment Facilities.  West Chester, Pennsylvania.  January 1970.
                                        73

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                                    TECHNICAL REPORT DATA
                            (Please read Instructions on the reverse before completing)
1. REPORT NO.
  EPA-600/2-76-294
                              2.
                                                            3. RECIPIENT'S ACCESSION-NO.
4. TITLE AND SUBTITLE
 Treatment of Effluent Waters from Vegetable Oil
 Refining
             5. REPORT DATE
             December 1976 (Issuing  date)
             6. PERFORMING ORGANIZATION CODE
7. AUTHOR(S)
 Gill,  D.  F.  and lelase,  J.  C.
                                                            8. PERFORMING ORGANIZATION REPORT NO.
9. PERFORMING ORGANIZATION NAME AND ADDRESS
 Archer  Daniels Midland Co.
 4666  Paries Parkway
 Decatur,  IL 62525
             10. PROGRAM ELEMENT NO.

                1BB037 ROAP 21  BAA Task 20
             11. CONTRACT/GRANT NO.

                12060 FDK
12. SPONSORING AGENCY NAME AND ADDRESS
 Industrial Environmental  Research Laboratory - Gin., OH
 Office  of Research and Development
 U.S.  Environmental Protection Agency
 Cincinnati,  OH  45268
             13. TYPE OF REPORT AND PERIOD COVERED
                Final	
             14. SPONSORING AGENCY CODE

                  EPA/600/12
15. SUPPLEMENTARY NOTES
16. ABSTRACT
 A detailed investigation was done to characterize the wastewater from a vegetable
 oil refinery.   A calcium chloride chemical  treatment was  installed which resulted
 in a net  decrease in waste  load of 71 percent from .0135  Ib  BOD5 per pound oil
 processed to .0039 Ib BOD5  per pound oil processed.  A further reduction of  50
 percent to .0019 Ib BOD  per pound oil processed was made by the addition of a
 clarifier to the treatment  system.  The net cost of treatment depends on the
 market value of the oil recovered and will  range from $.032  per pound processed
 to a gain of $.063 per pound oil processed
17.
                                KEY WORDS AND DOCUMENT ANALYSIS
                  DESCRIPTORS
                                               b.lDENTIFIERS/OPEN ENDED TERMS
                           c.  COSATI Field/Group
 Clarification
 Precipitation (Chemistry)
 Refining
 Vegetable Oils
 Waste Treatment
 Chemical Removal (Water Treatment)
  Vegetable Wastes,
  Economics, Vegetable
  Industry, Treatment
  Costs
   13B
    7A
    6H
   13H
18. DISTRIBUTION STATEMENT

 Release to  Public
19. SECURITY CLASS (ThisReport)
   UNCLASSIFIED
21. NO. OF PAGES

    89
                                               20. SECURITY CLASS (Thispage)
                                                 UNCLASSIFIED
                                                                          22. PRICE
EPA Form 2220-1 (9-73)
                                             79
                                                     U.S. GOVERNMENT PRINTING OFFICE: 1977-757-056/5577 Region No. 5'H

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