SUMMARY REPORT - FLUE GAS DESULFURIZATION. SYSTEMS - NOVEMBER - DECEMBER  1976
TnBLL                                                                                   PAGE
  1   SUMARY LIST OF FGD SYSTEMS                                                          3
  2   STATUS OF FGD SYSTEMS                                                                9
  3   PLKFOKMAKCL DESCRIPTION FUR OPERATIONAL FGD SYSTEMS                                 37
  H   NUMBER AIMD TOTAL MW UF FGL SYSTEMS                                                 195
  5   SUGARY oF FbU SYSTEMS BY COMPANY                                                  199
  fo   SUMMARY OF FGU SYSTEMS BY VENDOR                                                   203
  7   SUK'-'AKY UF NEW AND RETROFIT FGD SYSTEMS BY PROCESS                                 209
  6   SUGARY OF OPERATING FbU SYSTEMS BY PROCESS AND  GENERATING  UNITS                   213
  9   SUMMARY UF SLUUGE DISPOSAL PRACTICES FOR OPERATIONAL  FGu  SYSTEMS                   217
 lffr'  SUGARY UF FGD SYSTEMS BY PROCESS AND REGULATORY CLASS                             221
 11   SUMMARY OF OPERATIONAL FGD SYSTEhS                                                 227
 12   SUMf'.AKY OF FGU SYSTEMS UIVDER CONSTRUCTION                                          231
 13   SUMARY CF PLANNED FbD SYSTEMS                                                     237
 IH   SUMMARY LIST OF FGD SYSTEMS IN ThE EARLY PLANNING STAGES
 15   STATUS Op FGD SYSTEMS IN THE EARLY PLANNING STAGES
      FbD SYSTLM OPERATIONS THAT HAVE BEEN TERMINATED  OR SHUT DOWN  INDEFINITELY  APPENDIX  A
      FGD ECONOMICS                                                              APPENDIX  B
      FGU PROCESS FLOW OIAbRAMS                                                  APPENDIX  C
      DEFINITIONS                                                                APPENDIX  D
       PREPARED BY
PEDCO-ENVIRONMENTAL INC.
     H495I CHESTER ROAD
 CINCINNATI, OHIO
DIVISION OF
ENFORCEMENT
               PREPARED FOR
             STATIONARY SOURCE
                   AND
INDUSTRIAL ENVIRONMENTAL RESEARCH LABORATORY
   U.S.  ENVIRONMENTAL PROTECTION AGENCY
            RESEARCH TRIANGLE PARK,
             NORTH CAROLNA  27711
                                    CONTRACT NO. 68-02-1321
                                          TASK NO. 28

-------
         TABLE  1




SUMMARY LIST OF FGD SYSTEMS
                                 PEDCO-ENVIRONMENTAL

-------
PEOCO ENVIRONMENTAL

-------
                                          TABLE  1
                               SUMMARY  LIST  OF FGD  SYSTEMS
  FGO  STATUS  REPORT  12/76

  1.0.  NUMBER AND  COMPANY  NAME
    UNIT NAME
            LOCATION
START UP DATE   STATUS
       RE6
       CLASS
    1  ALABAMA  ELECTRIC  COOP
    2  ALABAMA  ELECTRIC  COOP
    3  ALLEGHENY  POWER SYSTEM
    4  ALLEGHENY  POWER SYSTEM
    5  ARIZONA  ELECTRIC  POWER COOP
    6  ARIZONA  ELECTRIC  POWER COOP
    7  ARIZONA  PUbLlC SERVICE
    8  AKIZONA  PUBLIC SERVICE
    9  ARIZONA  PUBLIC SERVICE
   10  AKIZONA  PUBLIC SERVICE
   11  ARIZONA  PUbLlC SERVICE
   12  BASIN ELECTRIC POWER COOP
   13  BASIN ELECTRIC POWtR COOP
   14  BASIN ELECTRIC POWER COOP
   15  faASIN ELECTRIC POWER COOP
   16  BASIN ELECTRIC POWER COOP
   17  BIG RIVERS ELECTRIC COOP CORP.
   18  BRAZOS ELECTRIC POWER COOP
   19  CENTRAL  ILLINOIS  LIGHT CO.
   20  CENTHAL  ILLINOIS  LIGHT CO.
   21  CENTRAL  ILLINOIS  LIGHT CO.
   22  CENTRAL  ILLINOIS  PUBLIC SERV
   23  CINCINNATI GAS 8  ELECTRIC CO,
   24  COLORADO UTE ELECTRICAL ASSN.
   25  COLORADO UTE ELECTRICAL ASSN.
   26  COLUMBUS & SOUTHERN OHIO ELEC.
   27  COLUMBUS & SOUTHERN OHIO ELEC.
   28  COLUMBUS & SOUTHERN OHIO ELEC.
   29  COLUMBUS & SOUTHERN OHIO ELEC.
   30  COMMONWEALTH EDISON
   31  COMMONWEALTH EDISON
   32  DETROIT  EDISON
   33  GUflUESNE LIGHT
   34  OUQUESNE LIGHT
   35  EASTERN  KENTUCKY  POWER COOP
 TOMBIGBEE NO.  2
 TOMBIGBEE NO.  3
 PLEASANTS NO.  I
 PLEASANTS NO.  2
 APACHE NO 2
 APACHE NO 3
 ChOLLA NO 1
 CHOLLA NO 2
 FOUR CORNERS NO.  «f
 FOUK CORNERS NO.  SA
 FOUR CORNERS NO.  SB
 ANTELOPE VALLEY NO. 1
 ANTELOPE VALLEY NO. 2
 MISSOURI BASIN NO 1
 MISSOURI BASIN NO 2
 MISSOURI BASIN NO 3
 RLIU STEAM STATION NO.  2
 ATACOSA MCMULLEN NO. 1
 DUCK CREEK NO. 1A
 DUCK CREEK NO. IB
 DUCK CREEK NO.2
 NEWTON NO.l
 EAST BEND NO 2
 CRAIG STATION NO.l
 CRAIG STATION NO.2
 CONESVILLE NO 5
 CONESVILLE NO 6
 POSTON NO. 5
 POSTON NO. 6
 POuJtRTON NO. 51
 WILL COUNTY NO 1
 ST. CLAIR NO 6
 ELRAMA POWER STATION
 PHILLIPS POWER STATION
 SPUKLOCK GENERATING PLANT
     JACKSON ALABAMA
     JACKSON ALABAMA
     BELLMONT W VIRGINIA
     BELLMONT W VIRGINIA
     COCHISE ARIZONA
     COCHISE ARIZONA
     JOSEPH CITY ARIZONA
     JOSEPH CITY AKIZONA
     FARMINGTON NEW MEXICO
     FARMINGTON NEW MEXICO
     FARMINGTON NEW MEXICO
     BEULAH  NORTH DAKOTA
     BEULAH  NORTH DAKOTA
     WHEATLAND WYOMING
     WHEATLAND WYOMING
     WHEATLAND WYOMING
     SEBREL KENTUCKY
     SAN MIGUEL  TEXAS
     CANTON ILLINOIS
     CANTON ILLINOIS
     CANTON ILLINOIS
     NEUTON ILLINOIS
     RABBIT HASH KENTUCKY
     CRAIG COLORADO
     CRAIG COLORADO
     CONL'SVILLE OHIO
     CONESVILLE OHIO
     ATHENS OHIO
     ATHENS OHIO
     PEKIN  ILLINOIS
     ROMEOVILLE ILLINOIS
     BELLE RIVER MICHIGAN
     ELRAMA PENNSYLVANIA
     SOUTH HEIGHT PENNSYLVANIA
NO.2 MAYSVILLE KENTUCKY
1.  OPERATIONAL UNITS           4.
2.  UNITS UNDER CONSTRUCTION    5.
3.  PLANNED - CONTRACT AWARDED  6.
PLANNED - LETTER OF INTENT SIGNED
PLANNED - REQUESTING/EVALUATING BIDS
CONSIDERING ONLY FGD SYSTEMS
       3-78
       3-79
       3-79
       3.80
       6-78
       6-79
      10-73
       6-77
       0- 0
       2-76
       0- 0
       0-81
       0-64
       4-80
      10-80
       6-63
      12-79
      12-79
       9-76
       8-78
       1-62
       7-76
       1-81
       3-79
       3-79
       2-77
       1-78
       0-81
       0-83
      12-79
       2-72
       5-76
      10-75
       7-73
       3-80
2
2
2
2
2
2
1
2
6
1
6
6
6
3
3
6
2
3
1
2
6
2
6
6
6
2
3
6
6
3
1
1
1
1
6
A
A
A
A
B
B
B
B
B
B
B
8
B
B
B
6
A
E
A
A
A
A
A
B
B
B
B
B
B
C
C
C
B
B
A
A.  BOILER CONSTRUCTED SUBJECT TO FEDERAL NSPS
B.  BOILER SUBJECT TO STATE STANDARD THAT IS MORE STRINGENT THAN THE FEDERAL NSPS
C.  BOILER SUBJECT TO STATE STANDARD THAT IS EQUAL TO OR LESS STRINGENT THAN NSPS
D.  OTHER
E.  REGULATORY CLASS UNKNOWN
                                                                                                PEDCO ENVIRONMENTAL

-------
                                          TABLE 1
                               SUMMARY LIST OF FGD SYSTEMS
  F6D STATUS REPORT 12/76

  I.D. NUMBER ANQ COMPANY NAME
    UNIT NAME
       LOCATION
START UP DATE   STATUS
                                                                                                                          RE6
                                                                                                                          CLASS
   36 GENERAL MOTORS
   37 GULF POWER CO.
   38 INDIANAPOLIS POWER & LIGHT CO.
   39 INDIANAPOLIS POWER & LIGHT CO.
   
-------
                                          TABLE 1
                               SUMMARY  LIST  OF FGD SYSTEMS
  FGD  STATUS  REPORT  12/76

  I.D.  NUMBER AND  COMPANY NAME
    UNIT NAME
       LOCATION
START UP DATE   STATUS
       REG
       CLASS
   71  NEVADA  POWER
   72  NEVADA  POWER
   73  NEW ENGLAND ELEC SYSTEM
   7
-------
                                          TABLE 1
                               SUMMARY  LIST  OF  FGO SYSTEMS
  FGO STATUS REPORT  12/76

  1.0.  NUMBER AND COMPANY NAME
    UNIT NAME
       LOCATION
START UP DATE   STATUS
       RES
       CLASS
  106 SOUTHERN CALIFORNIA EDISON
  107 SOUTHERN ILLINOIS POWER  COOP
  106 SOUTHERN INDIANA GAS&ELECTRIC
  109 SOUTHERN MISSISSIPPI ELECTRIC
  110 SOUTHERN MISSISSIPPI ELECTRIC
  111 SPRINGFIELD CITY UTILITIES
  112 TENNESSEE VALLEY AUTHORITY
  113 TENNESSEE VALLEY AUTHORITY
  lit TENNESSEE VALLEY AUTHORITY
  115 TEXAS UTILITIES CO.
  116 TEXAS UTILITIES CO.
  117 TEXAS UTILITIES CO.
  116 TEXAS UTILITIES CO.
  119 TEXAS UTILITIES CO.
  120 UIJITED POWER ASSOCIATION
  121 UNITED POWER ASSOCIATION
  122 UTAH POWEK i LIGHT CO.
  123 UTAH POWER & LIGHT CO.
  12<* WISCONSIN POWEK & LIGHT  CO.
 MOHAVE NO.  2
 SOUTHERN ILLINOIS POWER PT.
 A.B.  BROWN  .JO.l
 R.O.  MORROW NO.l
 R.D.  MORROW NO.2
 SOUTHWEST NO. 1
 SHAWNEE N0.10A
 SHAWNEE N0.10B
 WIDOWS CREEK NO 6
 MARTIN LAKE NO. 1
 MARTIN LAKE NO. 2
 MARTIN LAKE NO. 3
 MAKTIN LAKE NO. H
 MONTICELLO  NO.3
 COAL  CREEK  NO. 1
 COAL  CREEK  NO. 2
 EfiEKY NO.l
 HUNTINGTON  NO.l
 COLUMBIA NO. 2
LAUGHLIN NEVADA
MARION  ILLINOIS
WEST FRANKLIN INDIANA
HATTIESBURG MISSISSIPPI
HATTIESBURG MISSISSIPPI
SPRINGFIELD MISSOURI
PADUCAH KENTUCKY
PADUCAH KENTUCKY
BRIDGEPORT ALABAMA
TATUM TEXAS
TATUM TEXAS
TATUM  TEXAS
TATUM  TEXAS
MT. PLEASANT TEXAS
UNDERWOOD NORTH DAKOTA
UNDERWOOD NORTH DAKOTA
EMEKY COUNTY  UTAH
PRICE UTAH
PORTAGE  WISCONSIN
       6-77
       1-78
       H-79
      11-77
       6-78
       2-77
       «f-72
       «»-72
       3-77
       1-77
      10-77
      12-78
      12-79
      10-77
      11-78
      11-79
       6-78
       6-77
       1-80
6
3
3
2
2
2
1
1
2
2
2
3
3
2
3
3
3
2
5
E
A
A
A
A
A
C
C
C
A
A
A
A
A
A
A
A
A
A
1.  OPERATIONAL UNITS           «».
2.  UNITS UNDER CONSTRUCTION    5.
3.  PLANNED - CONTRACT AWARDED  6.
PLANNED - LETTER OF INTENT SIGNED
PLANNED - REQUESTING/EVALUATING BIDS
CONSIDERING ONLY FGO SYSTEMS
A.  BOILER CONSTRUCTED SUBJECT TO FEDERAL NSPS
B.  BOILER SUBJECT To STATE STANDARD THAT IS MORE STRINGENT THAN THE FEDERAL NSPS
C.  BOILER SUBJECT To STATE STANDARD THAT IS EQUAL To OR LESS STRINGENT THAN NSPS
D.  OTHER
E.  REGULATORY CLASS UNKNOWN
                                                                                                PEDCO ENVIRONMENTAL

-------
      TABLE  2



STATUS OF FGD SYSTEMS
                              PEDCO-ENVIRONMENTAL

-------
10                                PEUCO ENVIRONMENTAL

-------
 COMPANY
           TABLE 2
STATUS OF FGD SYSTEMS DURING  12/76
 POWER STATION
                       CURRENT MONTH
I.D. NUMBER    1
ALABAMA ELECTRIC COOP
TOMBIGBEE NO. 2
  225  MW - NEW
COAL   O.b- 1.5 PERCENT SULFUR
PEABOOY ENGINEERING
LIMESTONE. SCRUBBING
STARTUP   3/7«
    PEABOOY ENGINEERING HAS BEEN AWARDED THE CONTRACT FOR THE INSTALLATION
    OF A LIMESTONE SCRUBBING SYSTEM ON THIS UNIT.  A HIGH-EFFICIENCY ESP WILL
    BE INSTALLED UPSTREAM OF THE SCRUBBING SYSTEM  TO PROVIDE PRIMARY
    PARTICULATE CONTROL. THE FGD SYSTEM CONTAINS TWO SCRUBBING TRAINS.
    TREATING APPROXIMATELY 70 PERCENT  OF THE FLUE  GAS FOR REMOVAL OF SULFUR
    DIOXIDE. STACK GAS REHEAT WILL NOT BE REQUIRED. DURING THE REPORT PERIOD*
    WORK ON THE CONSTRUCTION OF THIS UNIT CONTINUED. SITE PREPARATION
    AMU FOUNDATION WORK HAVE BEEN COMPLETED.EQUIPMENT ERECTION IS PROCEEDING.
I.D. NUMBER    2
ALABAMA ELECTRIC COOP
TOMBIGBEE NO. 3
  225  fW - NEW
COAL   0.5- 1.5 PERCENT SULFUR
PEABODY ENGINEERING
LIMESTONE SCRUBBING
STARTUP   3/79
    PEABODY ENGINEERING HAS BEEN AWARDED THE CONTRACT FOK THE INSTALLATION
    OF A LIMESTONE SCRUBBING SYSTEM ON THIS UNIT. A HIGH-EFFICIENCY ESp WILL
    BE INSTALLED UPSTREAM OF THE SCRUBBING SYSTEM TO PROVIDE PRIMARY
    PARTICULATE CONTROL. THE FGO SYSTEM CONTAINS TWO SCRUBBING TRAINS.
    TREATING APPROXIMATELY 70 PERCENT OF THE FLUE GAS FOK REMOVAL OF SULFUR
    DIOXIDE. STACK GAS REHEAT WILL NOT BE REQUIRED. DURING THE REPORT PERIOD.
    WORK ON THE CONSTRUCTION OF THIS UNIT CONTINUED. SITE PREPARATION AND
    FOUNDATION WORK HAVE BEEN COMPLETED. EQUIPMENT ERECTION IS PROCEEDING.
I.D. NUMBER    3
ALLEGHENY POWER SYSTEM
PLEASANTS NO. 1
  625  MW - NEW
COAL H.5 PERCENT SULFUR  (MAX)
BABCOCK AND WlLCOX
LIME SCRUBBING
STARTUP   3/79
    THE THREE PRINCIPAL OPERATING UTILITY COMPANIES OF THE ALLEGHENY POWER
    SYSTEM ARE INSTALLING AN EMISSION CONTROL SYSTEM FOR THIS NEW COAL-FIRED
    UNIT WHICH INCLUDES A HIGH EFFICIENCY ESP UPSTREAM OF FOUR SPRAY TOWERS
    FOR THE CONTROL OF PARTICULATES AND SULFUR DIOXIDE. DESIGN REMOVAL
    EFFICIENCIES FOR THIS EMISSION CONTROL SYSTEM ARE 99.5 AND 90 PERCENT
    RESPECTIVELY. THE DRAVO CO. IS SUPPLYING THIOSORBIC LIME. THE CONSULTING
    ENGINEERING FIRM IS UNITED ENGINEERS AND CONSTRUCTORS. SLUDGE
    DISPOSAL PLANS ARE NOW BEING EVALUATED ANU FINALIZED.
1.0. NUMBER    «»
ALLEGHENY POWER SYSTEM
PLEASANTS NO. 2
  625  MW - NEW
COAL t.5 PERCENT SULFUR  (MAX)
BABCOCK AND WlLCOX
LIME SCRUBBING
STARTUP   3/60
    THE THREE PRINCIPAL OPERATING UTILITY COMPANIES OF THE ALLEGHENY POWER
    SYSTEM ARE INSTALLING AN EMISSION CONTROL SYSTEM FOR THIS NEW COAL-FIRED
    UNIT WHICH INCLUDES A HIGH EFFICIENCY ESP UPSTREAM OF FOUR SPRAY TOWERS
    FOR THE CONTROL OF PARTICULATES AND SULFUR DIOXIDE. DESIGN REMOVAL
    EFFICIENCIES FOR THIS EMISSION CONTROL SYSTEM ARE 99.5 AND 90 PERCENT.
    RESPECTIVELY. THE DRAVO CO. IS SUPPLYING THIOSORBIC LIME. THE CONSULTING
    ENGINEERING FIRM IS UNITED ENGINEERS AND CONSTRUCTORS.  SLUDGE
    DISPOSAL PLANS ARE NOW BEING EVALUATED AND FINALIZED.
I.D. NUMBER     5
ARIZONA ELECTRIC  POWER  COOP
APACHE NO 2
  200  KW -  NEW
COAL  0.5- O.fl  PERCENT  SULFUR
RESEARCH COTTRELL
LIMESTONE SCRUBBING
STARTUP   6/7fl
    THE CONTRACT FOR THE INSTALLATION OF A WET LIMESTONE SCRUBBING SYSTEM HAS
    BEEN AWARDED BY THE UTILITY TO RESEARCH-COTTRELL. CONSTRUCTION OF THE
    SYSTEM IS NOW IN PROGRESS. SITE PREPARATION AND FOUNDATION WORK IS
    NEARING COMPLETION. THE CONCRETE FOR THE SCRUBBING TOWER HAS ALREADY
    BEEN POURED. THE EMISSION CONTROL SYSTEM WILL CONSIST OF A HIGH-
    EFFICIENCY ESP INSTALLED UPSTREAM OF TWO PACKED TOWERS. GUARANTEED S02
    ANO PARTICULATE REMOVAL EFFICIENCIES ARE 85 AND 99.4 PERCENT.
    RESPECTIVELY. THE A-E UESIGN FIRM IS BURNS & MCDONNELL.
                                                                 1)
                                                                PEOCO ENVIRONMENTAL

-------
 COMPANY

 POWER STATION
           TABLE 2
STATUS OF FGD SYSTEMS DURING  12/76

                       CURRENT MONTH
1.0. NUMBER    6
ARIZONA ELECTRIC POWER COOP
APACHE NO 3
  200  MW - NEW
COAL   0.5- O.fl PERCENT SULFUR
RESEARCH COTTKELL
LIMESTONE SCRUBBING
STARTUP   6/79
    THE CONTRACT FOR THE INSTALLATION OF A WET LIMESTONE SCRUBBING SYSTEM HAS
    BEEN AWARDED BY THE UTILITY TO RESEARCH-COTTRELL. CONSTRUCTION OF THE
    SYSTEM IS NOW IN PROGRESS. SITE PREPARATION AND FOUNDATION WORK IS
    NEARING COMPLETION. THE CONCRETE FOR THE SCRUBBING TOWER HAS ALREADY
    BEEN POURED. THE EMISSION CONTROL SYSTEM WILL CONSIST OF A HIGH-
    EFFICIENCY ESP INSTALLED UPSTREAM OF TWO PACKED TOWERS, GUARANTEED S02
    AND PARTICULAR REMOVAL EFFICIENCIES ARE 85 AND 99.1 PERCENT,
    RESPECTIVELY. THL A-E. FIRM IS BURNS & MCDONNELL,
1.0. NUMBER    7
ARIZONA PUBLIC SERVICE
CHOLLA NO 1
  115  MW - RETROFIT
COAL   0.
-------
 COMPANY
 POWER STATION
           TABLE 2
STATUS OF F6D SYSTEMS DURING
       12/76

CURRENT MONTH
I.D. NUMBER   11
ARIZONA PUBLIC SERVICE
FOUR CORNERS NO. 58
  595  MW - RETROFIT
COAL  0.7 - 0.75S SULFUR  (AVG)
NOT SELECTED
NOT SELECTED
STARTUP   O/ 0
    THE BALANCE OF FLUE GAS FROM THE 755-HW  NO.5 UNIT  WILL  BE  CONTROLLED
    PENDING THE OUTCOME OF TESTS CURRENTLY BEING CONDUCTED  ON  THE PROTOTYPE
    PROTOTYPE WEIR HORIZONTAL SCRUBBING MODULE INSTALLED  ON THIS  UNIT.
    TEST RESULTS ON THE PROTOTYPE'S PERFORMANCE  WILL BE PUBLISHED IN
    FEBRUARY 1977. A DECISION CONCERNING SULFUR  DIOXIDE CONTROLS
    FOR THIS UNIT HAS NOT YET BEEN FINALIZED.
I.D. NUMBER   12
BASIN ELECTRIC POWER COOP
ANTELOPL VALLEY NO. 1
  «*50  Mta - NEW
LIGNITE 1.0 PERCENT SULFUR
NOT SELECTED
NOT SELECTED
STARTUP   0/81
    THE UTILITY IS CURRENTLY INVESTIGATING  VARIOUS FGD PROCESSES FOR TWO
    COAL-FIRED UNITS AT  THIS NEW STATION  WHICH WILL BE LOCATED IN MERCER
    COUNTY. NEAR BEULAHt  NORTH DAKOTA.  THIS NEW FACILITY  WILL BE KNOWN AS
    THE ANTELOPE VALLEY  STATION AND WILL  BE REQUIRED TO COMPLY WITH AIR
    EMISSION STANDARDS VIA THE BEST AVAILABLE TECHNOLOGY. START-UP IS NOW
    SCHEDULED FOR 1961.
I.D. NUMBER   13
BASIN ELECTRIC POWER COOP
ANTELOPE VALLEY NO. 2
  450  MW - NEW
LIGNITE 1.0 PERCENT SULFUR
NOT SELECTED
NOT SELECTED
STARTUP   0/8H
    THE UTILITY IS CURRENTLY INVESTIGATING VARIOUS FGD PROCESSES FOR TWO
    COAL-FIRED UNITS AT THIS NEW STATION WHICH WILL BE LOCATED IN MERCER
    COUNTY,NEAR BEULAH.NORTH DAKOTA.  THIS NEW FACILITY WILL BE KNOWN AS
    THE ANTELOPE VALLEY STATION AND WILL BE REQUIRED TO COMPLY WITH AIR
    EMISSION STANDARDS VIA THE BEST AVAILABLE TECHNOLOGY•  START-UP IS NOW
    SCHEDULED FOR
I.D. NUMBER   If
BASIN ELECTRIC POWER COOP
MISSOURI BASIN NO  1
  550  MW - NEW
LIGNITE 0.6 PERCENT SULFUR
RESEARCH COTTREUL
LIMESTONE SCRUBBING
STARTUP   M/80
    BECAUSE OF THE STRICT STATE OF WYOMING EMISSION STANDARDS OF 0.2 LBS.
    OF S02 PER MILLION BTU HEAT INPUT*  LOl' SULFUR COAL ALONE WILL NOT MEET
    STANDARDS. DURING THE REPORT PERIOD THE UTILITY AWARDED A CONTRACT
    TO RESEARCH COTTRELL FOR THE INSTALLATION OF A LIMESTONE SCRUBBING
    SYSTEM ON THIS UNIT. THE UNIT IS DESIGNED TO FIRE LIGNITE HAVING A
    HEAT CONTENT OF 6000 BTU/LB AND ASH AND SULFUR CONTENTS OF
    7.0 AND 0.6 PERCENT* RESPECTIVELY.  THE A-E DESIGN FIKM IS
    BURNS a MCDONNELL.
I.D. NUMBER    15
BASIN ELECTRIC POWER  COOP
MISSOURI BASIN NO  2
  550  MW  -  NEW
COAL
RESEARCH COTTRELL
LIMESTONE  SCRUBBING
STARTUP  10/80
    BECAUSE OF THE STKICT STATE OF WYOMING EMISSION STANDARDS OF 0.2 LBS*
    OF S02 PER MILLION BTU HEAT INPUT* LOW SULFUR ALONE WILL NOT MEET
    STANDARDS. DURING THE REPORT PERIOD THE UTILITY AWARDED A CONTRACT
    TO RESEARCH COTTKELL FOR THE INSTALLATION OF A LIMESTONE SCRUBBING
    SYSTEM ON THIS UNIT. THE UNIT IS DESIGNED TO FIRE LIGNITE HAVING A
    HEAT CONTENT OF 6000 BTU/LB AND ASH AND SULFUR CONTENTS OF
    7.0 AND 0.6 PERCENT* RESPECTIVELY. THE A-E DESIGN FIKH IS
    BURNS & MCDONNELL.
                                                                                                  PEDCO CNVXRONRCNTAL

-------
 COMPANY

 POWER STATION
           TABLE 2
STATUS OF FSO SYSTEMS DURING  12/76

                       CURRENT MONTH
1.0. NUMBER   16
BASIN ELECTRIC POWER COOP
MISSOURI BASIN NO 3
  550  MW - NEW
COAL
NOT SELECTED
NOT SELECTED
STARTUP   6/83
    BECAUSE OF THE STRICT STATE OF WYOMING EMISSION STANDARDS OF 0*2 LBS.
    S02 PER MILLION BTU HEAT INPUT, LOW SULFUR COAL ALONE WILL NOT MEET
    STANDARDS. THE UTILITY IS CURRENTLY INVESTIGATING VARIOUS FGD PROCESSES
    FOR THE NO.3 UNIT AT THE MISSOURI BASIN STATION.
I.D. NUMBER   17
BIG RIVERS ELECTRIC COOP CORP,
REID STEAM STATION NO. 2
  250  MM - NEW
COAL 3.5-1.0 PERCENT SULFUR
AMERICAN AIM FILTER
LIME SCRUBBING
STARTUP  12/79
    THE UTILITY HAS AWARDED A CONTRACT TO THE AMERICAN AIR FILTER COMPANY
    FOR THE INSTALLATION OF AN EMISSION CONTROL SYSTEM ON THIS NEW COAL-FIRED
    UNIT LOCATED IN SEBREE. KENTUCKY. AAF WILL DESIGN,FABRICATE AND INSTALL
    AN ESP AND TWO SPRAY TOWERS FOR THE CONTROL OF PARTICULATES AND SULFUR
    DIOXIDE.DESIGN REMOVAL EFFICIENCIES ARE 99.6 AND 90 PERCENT RESPECTIVELY.
    THE BOILER, WHICH IS CURRENTLY UNDER CONSTRUCTION, WILL FIRE HIGH SULFUR
    WESTERN KENTUCKY COAL  (3.5 TO <».5 PERCENT) AND COMPLY WITH NEW SOURCE
    PERFORMANCE STANDARDS.CONSTRUCTION OF THE CONTROL SYSTEM IS NOW UNDERWAY,
I.D. NUMBER   16
BRAZOS ELECTRIC POWER COOP
ATACOSA MCKULLEN NO. 1
  HOO  MW . NEW
LIGNITE 1.67 PERCENT SULFUR
BABCOCK & WILCOX
LIMESTONE SCRUBBING
STARTUP  12/79
    BAbCOCK AND WILCOX HAS BEEN AWARDED THE CONTRACT FOR THE INSTALLATION OF
    THIS ENTIRE MEw SYSTEM. THE. EMISSION CONTROL EQUIPMENT FOR THE COAL-FIRED
    RADIANT BOILER WILL CONSIST OF ELECTROSTATIC PRECIPITATORS UPSTiHEAM OF
    THE LIMESTONE SCRUBBING MODULES. THE SCRUBBER FLUE GAS CAPACITY IS
    NOMINALLY DESIGNED TO LXCELD 1.5 MILLION ACFM. THE OLSIGN S02 REMOVAL
    EFFICIENCY IS 66 PERCENT FOR <»tOO PPM S02 INLET. LIGNITE COAL WILL BE
    FIKED Iivl THE BOILER. THE SCRUBBING WASTES WILL BE DISPOSED IN AN OFF-
    SITE MINEFILL. THE CONSULTING A-E FIRM IS TIPPETT AND GEE.
I.D. NUMBER   19
CENTRAL ILLINOIS LIGHT CO.
DUCK CREEK NO. 1A
  100  MW - NEW
COAL 2.5 - 3.0 PERCENT SULFUR
RILEY STOKER / ENVlRONEERING
LIMESTONE SCRUBBING
STARTUP   9/76
    THE INSTALLATION OF THIS SINGLE 100-MW SCRUBBER MODULE WAS COMPLETED IN
    JULY AND START-UP OPERATIOIJS FOLLOWED, DEBUGGING OPERATIONS HAVE BEEN
    PROCEEDING ON AN INTLRhlTTLwT BASIS BECAUSE OF CONSTRUCTION-RELATED
    PROBLEMS. THE SYSTEM WAS SHUTDOWN FOR A SHORT PERIOD OF TIME TO CORRECT
    THLSE PROBLEMS. RE-START COMMENCED ON SEPTEMBER 9. OPERATION OF THE
    MOuULE DURLMG THE PERIOD FOLLOWING START-UP HAS BEEN INTERMITTENT BECAUSE
    OF McCHAMCAL AND CHEMICAL-RELATED PROBLEMS. THIS HAS PROMPTED THE
    UTILITY TO SHUTDOWN THE MODULE UNTIL FULL-SCALE START-UP DATE OF S/78.
I.D. NUMBER   20
CENTRAL ILLINOIS LIGHT CO.
DUCK CRELK NO. IB
  300  MW - NEW
COAL 2.5 - 3,0 PERCENT SULFUR
RILEY STOKER / ENVlRONEERING
LIMESTONE SCRUBBING
STARTUP   8/78
    A CONTRACT  HAS BEEN AWARDED BY THE UTILITY TO THE RILEY STOKER CORP. FOR
    THE OESIGN,  FABRICATION AND INSTALLATION OF THREE ADDITIONAL SCRUBBER
    MODULES FOR  THE BALANCE OF THIS UNIT. THE THREE MODULES HILL COMPLETE A
    FOUR MODULE  SULFUK DIOXIDE SCRUBBING SYSTEM, THE FIRST OF WHICH WAS
    PLACED IN SERVICE ON SEPTEMBER 9,1976. THE EMISSION CONTROL SYSTEM FOR
    THIS UNIT WILL CONSIST OF A HIGH-EFFICIENCY ESP UPSTREAM OF FOUR VENTRI-
    SORBER SCRUBBER MODULES. DESIGN PARTICULATE AND SULFUR DIOXIDE REMOVAL
    EFFICIENCIES AKE 99.8 AND 75 PERCENT.RESPECTIVELY.
                                                                                                  PCOCO ENVIRONMENTAL

-------
 COMPANY

 POWER STATION
           TABLE 2
STATUS OF FGO SYSTEMS DURING  12/76

                       CURRENT MONTH
I.D. NUMBER   21
CENTRAL ILLINOIS LIGHT CO.
3UCK CREEK NO.2
  400  MW - NEW
COAL 2.5-3.0 PERCENT SULFUR
AlOT SELECTED
.IMESTONE SCRUBBING
iTARTUP   1/82
    THE PROPOSED LIMESTONE SCRUBBING SYSTEM FOR THIS NEW COAL-FIRED
    UNIT IS SCHEDULED TO COMMENCE OPERATIONS IN JANUARY 1962.  THE
    UTILITY HAS NOT YET SELECTED A SYSTEM SUPPLIER. A DECISION CONCERNING
    THE. STATUS OF THE bOILLR AND CONTROL STRATEGY WILL BE
    ANNOUNCED IN LATE 1977.
I.D. NUMBER   22
:ENTRAL ILLINOIS PUBLIC SERV
JEWTON NO.l
  575  MW - NEW
:OAL 2.8-3.2 PERCENT SULFUR
•JUELL/ENVIROTECH
OOU3LE ALKALI SCRUBBING
•STARTUP   7/78
    A CONTRACT HAS BEEN AWARDED BY CIPSCO TO BUELL/ENVIROTECH FOR THE
    INSTALLATION OF AN EMISSION CONTROL SYSTEM ON UNIT N0.lt  A COAL-FIRED
    57b-MW POWER BOILER LOCATED IN NEWTONtILLINOIS. THE KEY COMPONENTS OF THE
    EMISSION CONTROL SYSTEM INCLUDE* A HIGH-EFFICIENCY ESP, FOUR SCRUBBER-
    ABSORBER TRAINS. THREE THICKENERS. TWO EXPERIMENTAL REHEAT SYSTEMS, AND
    THKEE HORIZONTAL EXTRACTION FILTERS FOR SLUUGE DENATURING. DESIGN PLANS
    CALL FOR COMPLETE WATER RECOVERY WITH ZERO EFFLUENT DISCHARGE. DESIGN
    PART1CULATE AND S02 REMOVAL EFFICIENCIES ARE 99.5 ANU 95 S,RESPECTIVELY.
t.D. NUMbER   23
CINCINNATI GAS & ELECTRIC CO.
'CAST 8ENO NO 2
  600  MW - NEW
COAL
HOT SELECTED
NOT SELECTED
STARTUP   1/81
    BIO REQUEST AND EVALUATION IS SCHEDULED TO COMMENCE SHORTLY.
    CONSTRUCTION AND OPERATING PERMITS ARt BEING PROCURED. A COAL
    SOURCE AND SUPPLY HAS NOT BEEN FINALIZED. COMMERCIAL
    START-UP DATE HAS BEEN DELAYED ONE TEAR TO JANUARY 1981.
    THL A-E DESIGN FIRM IS SARGENT AND LUNDY.
C.D. NUMBER   2«*
COLORADO UTE ELECTRICAL ASSN.
CRAIG STATION NO.l
  450  MW - NEW
COAL 0.45 PERCENT SULFUR
HOT SELECTED
LIME/LIMESTONE SCRUBBING
iJTARTUP   3/79
    THIS NEW STATION IS A MINE MOUTH FACILITY CONTAINING TWO COAL-FIRED
    POWER GENERATING UNITS. THESE UNITS WILL FIRE COLORADO LOW-SULFUR SUB-
    BITUMINOUS COAL HAVING A HEAT CONTENT OF 9100 TO 10300 BTU/LB AND ASH
    ANU SULFUR CONTENTS OF 10 TO 12 PERCENT AND 0.45 PERCENT, RESPECTIVELY.
    THE UTILITY IS NOW INVESTIGATING VARIOUS CONTROL STRATEGIES WHICH WILL
    PROBABLY INCLUDE HOT-SIDE ESP'S UPSTREAM OF WET CALCIUM-BASED SCRUBBERS.
    REQUIRED PARTICULATE AND SULFUR DIOXIDE REMOVAL EFFICIENCIES ARE 99.8
    AND 05 PERCENT, RESPECTIVELY. FGD START-UP IS SCHEDULED FOR SPRING 1979.
I.D. NUMBER   25
COLORADO UTE ELECTRICAL  ASSN.
CRAIG STATION NO.2
  450  MW - NEW
COAL 0.45 PERCENT SULFUR
MOT SELECTED
LIME/LIMESTONE SCRUBBING
STARTUP   3/79
    THIS NEW STATION IS A MINE MOUTH FACILITY CONTAINING TWO COAL-FIRED
    POWER GENERATING UNITS. THESE UMTS WILL FIRE COLORADO LOW-SULFUR SUB-
    BITUMINOUS COAL HAVING A HEAT CONTENT OF 9100 TO 10300 BTU/LB AND ASH
    AND SULFUR CONTENTS OF 10 TO 12 PERCENT AND 0.45 PERCENT, RESPECTIVELY,
    THL UTILITY IS NOW INVESTIGATING VAKIOUS CONTROL STRATEGIES WHICH WILL
    PROBABLY INCLUDE HOT-SIOE ESP'S UPSTREAM OF WET CALCIUh-BASEO SCRUBBERS.
    REQUIRED PARTICULATE AND SULFUR DIOXIDL REMOVAL EFFICIENCIES ARE 99.8
    ANU 65 PERCENT, RESPECTIVELY. FGD STAKT-UP IS SCHEDULED FOK SPKING 1979.
                                                                15
                                                                PEDCO ENVIRONMENTAL

-------
 COMPANY

 POWER STATION
           TABLE 2
STATUS OF FGO SYSTEMS DURING
       12/76

CURRENT MONTH
1.0. NUMBER   26
COLUMBUS & SOUTHERN OHIO ELEC.
CONESVILLE NO 5
  400  MM - NEW
COAL  <».5 - <».9 PERCENT SULFUR
UNIVERSAL OIL PRODUCTS
LIME SCRUBBING
STARTUP   2/77
    THE CONSTRUCTION OF THE BOILER AND ESP HAVE BEEN COMPLETED. THE UNIT WAS
    PUT IN SERVICE IN SEPTEMBER AND HAS CONTINUED TO OPERATE WITH THE ESP
    IN THE FLUE GAS PATH. OPERATION OF THE A-SIOE SCRUBBING TRAIN HAS BEEN
    DELAYED BY A FIRE WHICH ORIGINATED INSIDE THE MODULE, RESULTING IN A
    PROJECTED MINIMUM DELAY PERIOD OF Six MONTHS. THE UTILITY IS NOW
    CONDUCTING AIR AhO WATER TESTS ON THE B-SIDE MODULE IN PREPARATION
    OF A FEBRUARY START-UP. THE DRAVO CORP. is SUPPLYING THIOSORBIC LIME. THE
    MINE MOUTH PLANT FIRES A HIGH SULFUR, HIGH ASH OHIO BITUMINOUS COAL.
I.D. NUMbER   27
COLUMBUS & SOUTHERN OHIO ELEC.
CONESVILLE NO 6
  tOO  MM • NEW
COAL  <».5 - 1.9 PERCENT SULFUR
UNIVERSAL OIL PRODUCTS
LIME SCRUBBING
STARTUP   1/78
    THE UTILITY SIGNED LONG-TEKM CONTRACTS WITH DRAVO FOR THE PURCHASE OF
    THIOSORBIC LIME AND KITH IUCS FOR THE PURCHASE OF SLUDGE FIXATIVES. CON-
    STRUCTION ON THIS UNIT IS CURRENTLY SCHEDULED FOR 1977 WITH COMPLETION
    EXPECTED BY JANUARY 1978. SIMILAR TO CONESVILLE NO.5, THIS MINE MOUTH
    PLANT WILL 3UhN COAL WITH 17 PERCENT ASH CONTENT AND f.5 TO H.9 PtRCENT
    SULFUR CONTENT. AN ELECTROSTATIC PKtClPITATOR WILL BE INSTALLED UPSTREAM
    OF THE F&O SYSTEM. THE A-E DESIGN FIRM IS BLACK AND VEATCH.
I.D. NUMBER   28
COLUMBUS & SOUTHERN OHIO ELEC.
POSTON NO. 5
  375  MW - NEW
COAL 2.5 PERCENT SULFUR
NOT SELECTED
NOT SELECTED
STARTUP   0/81
    THIS UNIT WILL BURN HIGH SULFUR OHIO COAL (APPROXIMATELY 2.5 PERCENT
    SULFUR CONTENT). THE DESIGN OF THE EMISSION CONTROL STRATEGY HAS
    NOT YET BEEN FINALIZED.
I.D. NUMBER   29
COLUMBUS S SOUTHERN OHIO ELEC.
POSTON NO. 6
  375  MW - NEW
COAL 2.5 PERCENT SULFUR
NOT SELECTED
NOT SELECTED
STARTUP   0/83
    THIS UNIT WILL BURN HIGH SULFUR COAL (APPROXIMATELY 2.5 PERCENT
    SULFUR CONTENT). THE DESIGN OF THE EMISSION CONTROL STRATEGY
    FOR THIS UNIT HAS NOT YET BEEN FINALIZED.
I.D. NUMbER   30
COMMONWEALTH EDISON
POWERTON NO. 51
  <*25  MW.- RETROFIT
COAL 3.6 PERCENT SULFUR
UNIVERSAL OIL PRODUCTS
LIMESTONE SCRUBBING
STARTUP  12/79
    THE CONTRACT FOR THIS FGO SYSTEM HAS BEEN AWARDED TO UNIVERSAL OIL
    PRODUCTS. THE PROCESS IS A CLOSED-LOOP WET LIMESTONE SCRUBBING SYSTEM
    WHICH WILL BE BACKFITTED TO BOILER 51, ONE OF TWO IDENTICAL BOILERS
    SUPPLYING STEAM TO AN 650 MW TURBINE-GENERATOR. THE FGD SYSTEM IS DE-
    SIGNED TO TREAT FLUE GAS RESULTING FROM THE COMBUSTION OF HIGH SULFUR
    COAL <3.6 PERCENT SULFUR* 8.3 PERCENT ASH* 17.3 PERCENT MOISTURE* 10,500
    BTU/LB.) AND ME.ET S02 EMISSION STANDARDS OF 1.8 LB. S02/MM BTU. THE
    TOTAL INSTALLED CAPITAL COST OF THE FGO SYSTEM IS ESTIMATED AT S50MM.
                                                                                                  PCOCO ENVIRONMENTAL

-------
 COMPANY

 POWER STATION
           TABLE 2
STATUS OF FGO SYSTEMS DURING  12/76

                       CURRENT MONTH
I.D..NUMBER   31
COMMONWEALTH EDISON
WILL COUNTY NO 1
  167  MW - RETROFIT
COAL 4.0 PERCENT SULFUR
BA&COCK & WILCOX
LIMESTONE SCRUBBING
STARTUP   2/72
    REFER TO THE BACKGROUND INFORMATION SECTION IN TABLE  3 OF  THIS REPORT.
    THIS FULL SCALE DEMONSTRATION SCRUBBING SYSTEM HAS BEEN IN SERVICE SINCE
    FEBRUARY 1972.  THE FGD SYSTEM INCLUDES TWO SCRUBBING  TRAINS FOR THE
    CONTROL OF PARTICULARS AND SULFUR DIOXIDE. MODULE AVAILABILITY*
    OPERABILITY, RELlABILITYt  AND UTILIZATION INDEX VALUES FOR THE PERIOD
    ARt POSTED IN TABLE THREE. THE BOILER FIRED BOTH LOW  SULFUR
    WESTERN COAL AND HIGH SULFUR ILLINOIS COAL DURING SEPARATE MONTHS.
    THE FlXATIOu AND HAULAWAY  OF SCRUBBtR WASTES CONTINUED DURING THE PERIOD,
I.D. NUMBER   32
DETROIT EDISON
ST. CLAIK NO 6
  163  MW - RETROFIT
COAL  3.7 PERCENT SULFUR
PEABOOY ENGINEERING
LIMESTONL SCRUBBING
STARTUP   5/76
    REFER TO THE BACKGROUND INFORMATION SECTION IN TABLE  3 OF THIS REPORT.
    A 30-DAY VENDOR QUALIFICATION RUN AND A WEEK-LONG FINAL ACCEPTANCE TEST
    WEHE SUCCESSFULLY  COMPLETED DUKING THE SPRING OF 1976. THE UTILITY IS
    NOW IN THE PROCESS OF CONDUCTING A MINIMUM TWO-MONTH  INTERNAL DEMONSTRA-
    TION PROGRAM DURING WHICH THE SCRUBBERS WILL OPERATE  IN THE S02-REMOVAL
    MODE. THIS PROGHAM IS BEING CONDUCTED PRIMARILY BY PLANT PERSONNEL.
    FOLLOWING COMPLETION OF THE S02 PROGRAM. THE VENTURI  SCRUBBERS WILL
    REMAIN IN THE FLUE GAS PATH, OPERATING IN THE PARTICULATE-REMOVAL MODE.
I.D. NUMBER   33
UUBUESNE LIGHT
ELRAMA POWER STATION
  510  MW - RETROFIT
COAL  1.0 - 2.8 PERCENT SULFUR
CHEMICO
LIKE SCRUBBING
STARTUP  10/75
    REFER TO THE BACKGROUND INFORMATION SECTION IN TABLE 3 OF THIS REPORT.
    THIS SCRUBBING SYSTEM•WHICH CONSISTS OF FIVE SINGLE-STAGE MODULES,WAS
    INITIALLY PLACED IN SERVICE OCTOBER 26,1975. INITIAL OPERATION PROCEEDED
    WITH FLUE GAS FROM ONE BOILER BEING TREATED BY FIVE SCRUBBING VESSELS.
    DUKING THE REPORT PERIOD OPERATIONS PROCEEDED WITH TWO BOILERS COUPLED
    INTO THE S-MODULE SCRUBBING SYSTEM. ONE SINGLE-STAGE SCRUBBING MODULE
    OPERATED WITH Two RUBBER-LINED RECYCLE PUMPS IN SERVICE. THE SCRUBBING
    WASTES ARE CHEMICALLY FIXATED BY THE IUCS METHOD AND LANOFILLED.
I.D. NUMBER   34
DUQUESNE LIGHT
PHILLIPS POWER STATION
  410  MW - RETROFIT
COAL   1.0- 2.6 PERCENT SULFUR
CHEMICO
LIME SCRUBBING
STARTUP   7/73
    REFER TO THE BACKGROUND INFORMATION SECTION IN TABLE 3 OF THIS REPORT.
    THIS SCRUBBING SYSTEM HAS BEEN IN SERVICE SINCE JULY 1973. THE UTILITY
    REPORTED THAT OPERATIONS DURING THE REPORT PERIOD WERE CONDUCTED WITH
    BOILER NOS. 2 THrtOUGH 6 COUPLED INTO THE SCRUBBING SYSTEM. BOILER NO.l
    REMAINED OUT OF SLrtVICE FOR OVERHAUL AND REPAIRS. THE IUCS INTERIM
    SCKUBBER SLUDGE PROCESSING PLANT IS NOW OPERATIONAL AT THE PLANT SITE.
    THE CHEMICALLY FIXED SLUDGE IS BEING DISPOSED IN AN OFF-SITE
    LANDFILL AREA.
I.D. NUMBER   35
EASTERN KENTUCKY POWER COOP
SPURLOCK GENERATING PLANT NO.2
  500  MW - NEW
COAL
NOT SELECTED
NOT SELECTED
STARTUP   3/80
    THE SPURLOCK GENERATING PLANT IS LOCATED APPROXIMATELY 3-MILES WEST OF
    MAYSVILLEiKENTUCKY. TWO NEW COAL-FIRED UNITS ARE SCHEDULED FOR THIS
    STATION. UNIT NO.l IS SCHEDULED FOR OPERATION IN MAY 1977. UNIT NO.2,
    WHICH WILL HAVE TO MEET NSPS, IS IN THE PLANNING STAGE. PARTlCULATES WILL
    BE CONTROLLED BY A 99.5 PERCENT EFFICIENT ESP. OESULFURIZATION MAY BE
    REGUIRED IF THE UTILITY CANNOT SECURE A LONG-TERM CONTRACT FOR THE
    PURCHASE OF LOW SULFUR COAL. A DECISION WILL BE MADE SOMETIME IN THE
    EARLT PART OF 1977.
                                                                17
                                                                PEOCO ENVIRONMENTAL

-------
 COMPANY

 POWER STATION
                                             TABLE 2
                                  STATUS OF F60 SYSTEMS DURING
       12/76

CURRENT MONTH
1.0. NUMBER   36
GENERAL MOTORS
CHEVROLET PARMA 1 2 3 & H
   32  MW - RETROFIT
COAL   2.5 PERCEMT SULFUR
KOCH/GENERAL MOTORS
DOUBLE ALKALI SCRUBBING
STARTUP   3/7H
                                      REFER TO BACKGROUND INFORMATION SECTION IN TABLE s OF THIS REPORT.
                                      THE EMISSION CONTROL SYSTEM FOR THESE 4-COAL FIRED STOKER BOILERS
                                      CONSISTS OF MECHANICAL COLLECTORS  INSTALLED UPSTREAM OF A DILUTE DOUBLE
                                      ALKALI SCRUBBING SYSTEM. THE FGO SYSTEM HAS BEEN IN SERVICE SINCE MARCH
                                      197
-------
 COMPANY

 POWER STATION
           TABLE 2
STATUS OF FGD SYSTEMS DURING  12/76

                       CURRENT MONTH
I.D. NUMBER   HI
KANSAS CITY POWER & LIGHT
HAWTHORN NO 4
  100  MW - RETROFIT
COAL   0.6- 3.0 PERCENT SULFUR
COMBUSTION ENGINEERING
LIMESTONE INJECTION *WET SCRUB
STARTUP   8/72
    REFER TO THE BACKGROUND INFORMATION SECTION IN TABLE 3 OF THIS REPORT.
    THIS INJECTION AND TAIL-END WET SCRUBBING SYSTEM WAS DESIGNED AND IN.
    STALLED BY COMBUSTION ENGINEERING AND PLACED IN SERVICE AUGUST 1972.
    FGO SYSTEM OPERATIONS DURING 1976 HAVE PROCEEDED ON AN INTERMITTENT
    BASIS. PROBLEMS ENCOUNTERED HAVE INCLUDED PLUGGING IN THE MARBLE BCD
    AND REHEAT TUBE BUNDLES, DRAFT LOSSES THROUGH THE DUCTWORK AND PUMP
    FAILURES. THE UTILITY IS NOW CONVERTING THIS SYSTEM FROM LIMESTONE
    INJECTION TO LIME INJECTION AND TAIL-END WET SCRUBBING.
I.D. NUMBER   42
KANSAS CITY POWER & LIGHT
LA CYGNE NO 1
  620  MW - NEW
COAL 5.0 PERCENT SuLFUR
BAfaCOCK * WILCOX
LIMESTONE SCRUBBING
STARTUP   2/73
    REFER TO THE BACKGROUND INFORMATION SECTION IN TABLE 3 OF THIS REPORT.
    THIS 7-MOOULE FGa SYSTEM HAS BEEN IN OPEKATION SINCE FEBRUARY 1973.
    THE ANNUAL SYSTEM OPERABILITY INDEX VALUE AVERAGED IN EXCESS OF
    76 PERCENT FOR 1974. ANNUAL AVERAGE AVAILABILITY INDEX VALUES FOR
    1975 AND 1976 EXCEEDED at PERCENT AND 91 PERCENT,RESPECTIVELY.
    THE NO.l UNIT WAS IN SERVICE THROUGHOUT THE REPORT PERIOD,
    ACHIEVING AVERAGE AVAILABILITY INDEX VALUES OF 94 AND 90 PERCENT FOR
    THt MONTHS OF NOVEMBER AND DECEMBER, RESPECTIVELY.
I.D. NUMBER   43
KANSAS POWER * LIGHT
JEFFERY NO. 1
  660  MW - NEW
COAL 0.32 PERCENT SULFUR
COMBUSTION ENGINEERING
LIMESTONE SCRUBBING
STARTUP   6/78
    THE UTILITY HAS PURCHASED AN AIR QUALITY CONTROL SYSTEM FROM COMBUSTION
    ENGINEERING FOR PARTICULATE AND S02 REMOVAL. THE SYSTEM WILL CONSIST OF
    AN ESP DOWNSTREAM OF THE AIR HEATER PLUS ID FANS AND SPRAY TOWERS. AN
    OVERFIRE AIR SYSTEM AT THE TANGENTIAL FIRED PULVERIZED BURNERS WILL CON-
    TROL THE NOX EMISSIONS. THE CLEANED GASES WILL BE VENTED TO A 600 FOOT
    STACK. THE CONSTRUCTION OF THIS NEW INSTALLATION IS PROCEEDING
    ACCORDING TO SCHEDULE. THIS UNIT WILL FIRE 250 TONS/HR OF WYOMING
    COAL WITH A HEAT CONTENT OF 8000 BTU/LB, 0.3* SULFUR AND 6X ASH.
I.D. NUMBER   44
KANSAS POWER & LIGHT
JEFFERY NO. 2
  6tiO  MW - NEW
COAL 0.32 PERCENT SULFUR
COMBUSTION ENGINEERING
LIMESTONE SCRUBBING
STARTUP   6/79
    THE UTILITY HAS PURCHASED AN AIR QUALITY CONTROL SYSTEM FROM COMBUSTION
    ENGINEERING FOR PAKTICULATE AND S02 REMOVAL. THE SYSTEM WILL CONSIST OF
    AN ESP DOWNSTREAM OF THE AIR HEATER PLUS ID FANS AND SPRAY TOWERS. AN
    OVERFIRE AIR SYSTEM AT THE TANGENTIAL FIRED PULVERIZED BURNERS WILL CON-
    TROL THE NOX EMISSIONS. THE CLEANED GASES WILL BE VENTED TO A 600 FOOT
    STACK. THE CONSTRUCTION OF THIS NE*I INSTALLATION IS PROCEEDING
    ACCORDING TO SCHEDULE. THIS UNIT HILL 250 TONS/HR OF WYOMING
    COAL HAVING A HEAT CONTENT OF UOOO BTU/LB, 0.3Si SULFUR ANO 68 ASH.
I.D. NUMBER   45
KANSAS POWER & LIGHT
LAWRENCE NO 4
  125  MW - RETROFIT
COAL 0.5 PERCENT  SULFUR
COKBUSTION ENGINEERING
LIMESTONE INJECTION *W£T  SCRUB
STARTUP  12/68
    REFER TO BACKGROUND INFORMATION SECTION IN TABLE 3 OF THIS REPORT.
    THE ORIGINAL FGD SYSTEM FOR THIS UNIT WAS PLACED IN SERVICE DECEMBER
    I960.  IN ACHIEVING AN OPTIMUM MODE OF OPERATION, THE PHYSICAL SCRUBBER
    PLANT WAS CONSUMED, REQUIRING REPLACEMENT WITH A NEW VENTUKl ROD
    SCRUBBER AND SPRAY TOWER ABSORBER SYSTEM SUPPLIED BY COMBUSTION
    ENGINEERING.INSTALLATION OF THE NEW SYSTEM IS COMPLETE.INITIAL OPERATION
    SHOULD COMMENCE IN THE EARLY PART OF 1977. THE UNIT WAS DOWN THROUGH*
    OUT THE KEPOHT PERIOD BECAUSE OF A SCHEDULED TURBINE OVERHAUL.
                                                                 19
                                                                PEOCO ENVIRONMENTAL

-------
 COMPANY

 POWER  STATION
           TABLE 2
STATUS OF FGO SYSTEMS QURINS  12/76

                       CURRENT MONTH
 1.0. NUMBER   if 6
 KANSAS  POWER X LIGHT
 LAWRENCE NO 5
  400   MU  - NEW
 COAL 0.5 PERCENT SULFUR
•COMBUSTION ENGINEERING
 LIMESTONE  INJECTION &WET  SCRUB
 STARTUP 11/71
    REFER TO BACKGROUND INFORMATION SECTION IN TABLE 3 OF THIS REPORT.
    THE ORIGINAL FGD SYSTEM FOR THIS UNIT WAS PLACED IN SERVICE NOVEMBER 1971
    RENTLY BURNING LOW SULFUR WYOMING COAL. THE OPERATION OF THE SCRUBBER HAS
    IN ACHIEVING AN OPTIMUM MODE OF OPERATION, THE PHYSICAL SCRUBBER PLANT
    WAS CONSUMEOi REQUIRING REPLACEMENT WITH TWO NEW VENTURI ROD
    SCRUBBERS AND SPRAY TOWER ABSORBERS SUPPLIED BY COMBUSTION ENGINEERING.
    IS PROCEEDING ON POURING OF THE FOUNDATION AND ERECTION OF THE
    STRUCTURAL STF.E.L.  THE BOILER IS IN SERVICE, FIRING FUEL OIL.
 I.D. NUMBER   i»7
 KENTUCKY UTILITIES
 GREEN RIVER   UNITS  1  AND
    6t  MW  - RETROFIT
 COAL  3.6  PERCENT SULFUR
 AMERICAN AIR  FILTER
 LIME SCRUBBING
 STARTUP    9/75
    REFER TO BACKGROUND INFORMATION SECTION IN TABLE 3 OF THIS REPORT,
    BOILERS 1, 2,  AND 3 ARE EXISTING UNITS WHICH HAVE BEEN FITTED WITH
    MECHANICAL COLLECTORS AND A WET LIME SCRUBBER-ABSORBER MODULE FOR
    THE CONTROL OF PARTICULATES AND SULFUR DIOXIDE.  THE SCRUBBER
    MODULE WAS ORIGINALLY PLACED IN THE FLUE 6AS PATH SEPT. 9, 1975.
    100,100,100, AND y"4 PERCENT RESPECTIVELY FOR THE MONTH OF OCTOBER.
    AN ANNUAL OPERABILITY INDEX VALUE OF 87 PERCENT.
 I.D. NUMBER   
-------
  COMPANY

  POWER STATION
           TABLE 2
STATUS OF FGD SYSTEMS DURING  12/76

                       CURRENT MONTH
'I.D. NUMBER   51
'LOUISVILLE GAS & ELECTRIC
'CANE RUN NO 6
   277  MW - RETROFIT
'COAL 3.5 - 4.0 PERCENT SULFUR
 AOL/COMBUSTION EQUIP ASSOCIATE
 DOUBLE ALKALI SCRUBBING
 STARTUP   2/79
    THE CONTRACT FOR  THIS FULL-SCALE DEMONSTRATION SCRUBBING  SYSTEM  HAS  BEEN
    AWARDED TO A.D.LITTLE/COMBUSTION EQUIPMENT  ASSOC.  FOR  THE INSTALLATION
    OF A DOUBLE ALKALI  SCRUBBER.  THE FEDERAL  EPA WILL  SUBSIDIZE  A  MAXIMUM
    Sif.5 MM FOR OPERATION*  RESEARCH AND DEVELOPMENTt AND REPORT  WRITING  FOR
    A ONE-YEAR PERIOD FOLLOWING THE FIRST  THREE MONTHS OF  OPERATION(NOTE*THIS
    SUBSIDY WILL NOT  BE APPLIED FOR ANY CAPITAL EXPENDITURES). ENGINEERING
    DESIGN WORK IS NOW  UNUEKWAY.  START-UP  IS  SCHEDULED FOK FEBRUARY  1.1979.
 I.D. NUMBER   52
 LOUISVILLE GAS i ELECTRIC
 MILL CREEK NO 1
   330  MW - RETROFIT
 COAL   3.5- 4.0 PERCENT SULFUR
 NOT SELECTED
 LIME: SCRUBBING
 STARTUP   1/82
    A COMPLIANCE SCHEDULE  HAS  BEEN SUBMITTED TO THE JEFFERSON  COUNTY  AIR  POL-
    LUTION CONTROL DISTRICT  WITH 1/82 ESTABLISHED AS THE  STARTUP  DATE FOR AN
    FGO SYSTEM.
'I.D. NUMBER   53
 LOUISVILLE GAS & ELECTRIC
 MILL CREEK NO 2
   330  MW - RETROFIT
 COAL   3.5- 4.0 PERCENT SULFUR
 NOT SELECTED
 LIME SCRUBBING
 STARTUP   1/el
    A COMPLIANCE SCHEDULE HAS BEEN SUBMITTED TO THE JEFFERSON COUNTY AIR  POL-
    LUTION CONTROL DISTRICT  WITH 1/81 ESTABLISHED AS THE STARTUP DATE FOR AN
    FGO SYSTEM.
 I.D. NUMBER   54
 LOUISVILLE GAS & ELECTRIC
 MILL CREEK NO 3
   425  MW - NEW
 COAL   3.5- 4.0 PERCENT SULFUR
 AMERICAN AIR FILTER
 LIME SCRUBBING
 STARTUP   7/77
    THE UTILITY HAS SIGNED A CONSENT AGREEMENT WITH THE EPA FOR THE INSTAL-
    LATION AND OPERATION OF FGO EQUIPMENT ON THIS POWER GENERATING UNIT  BY
    JULY 1.1977. THIS NEW FACILITY WILL BE REQUIRED TO MEET FEDERAL NSpS FOR
    THE LIMITATION OF S02 EMISSIONS. CONTRACT HAS BEEN AWARDED TO AMERICAN
    AIR FILTER. THE SYSTEM WILL OPERATE ON A CLOSED WATER LOOP AND THE SLUDGE
    WILL BE STABILIZED.  CONSTRUCTION HAS BEGUN ON THE FGD SYSTEM.
 I.D. NUMBER   55
 LOUISVILLE GAS & ELECTRIC
 MILL CREEK NO 4
   425  MW - NEW
 COAL   3.5- 4.0 PERCENT SULFUR
 AMERICAN AIR FILTER
 LIME SCRUBBING
 STARTUP   7/79
    THE UTILITY HAS SIGNED A CONSENT AGREEMENT WITH THE EPA FOR THE INSTAL-
    LATION AND OPERATION OF FGD EQUIPMENT ON THIS POWER GENERATING UNIT BY
    JULY 1.1979. THIS NEW FACILITY WILL BE REQUIRED TO MEET FEDERAL NSPS FOR
    THE LIMITATION OF S02 EMISSIONS. THE CONTRACT HAS BEEN AWARDED TO
    AMERICAN AIR FILTER FOR A LIME SCRUBBING SYSTEM.
                                                                 21
                                                                PEDCO ENVIRONMENTAL

-------
 COMPANY

 POWER STATION
           TABLE 2
STATUS OF FGD SYSTEMS DURING  12/76

                       CURRENT MONTH
1.0. NUMBER   56
LOUISVILLE GAS & ELECTRIC
PADDYS RUN NO 6
   65  MW - RETROFIT
COAL  3.5-i».0 PERCENT SULFUR
COMBUSTION ENGINEERING
LIME SCRUBBING
STARTUP   1/73
    REFER TO THE BACKGROUND INFORMATION SECTION IN TABLE 3 OF THIS REPORT.
    THIS SCRUBBING SYSTEM WAS DESIGNED BY COMBUSTION ENGINEERING AND PLACED
    IN SERVICE IN APRIL 1973. PADDYS RUN NO.6 IS A PEAK-LOAD UNIT THAT
    OPERATES ONLY DURING DEMAND PERIODS.  THE UNIT WAS OPERATIONAL DURING
    THE REPORT PERIOD. BEING AVAILABLE TO THE BOILER ON 99 PERCENT BASIS.
    SCKUbBER OPERATIONS WERE CONDUCTED ON CARBIDE LIME SLURRY DURING THE
    PERIOD.  THE EPA-SUBSIUI2EO SCRUBBER/SLUDGE STUDY CALLS FOR A HIGH
    CALCIUM VIRGIN LIME RUN TO COMMENCE ON MARCH 1, 1977.
I.D. NUMBER   57
MINNESOTA POWER AND LIGHT CO.
CLAY BOSWELL STATION N0.«t
  500  MW - NEW
COAL 0.8 PERCENT SULFUR
NOT SELECTED
MOT SELECTED
STARTUP   0/80
    THE UTILITY IS CURRENTLY REQUIESTING AND EVALUATING BIDS FOR THE INSTAL-
    LATION OF A SCRUBBING SYSTEM ON THIS NEW COAL-FIRED UNIT PLANNED FOR
    COMMERCIAL SERVICE IN THE SPRING OF 19BO. THIS NEW UNIT WILL FIRE LOW
    SULFUR SUBBITUMNOUS COLSThIP COAL. THE UTILITY IS CONSIDERING DRY
    COLLECTION AND MET SCRUBBING STRATEGIES (ESP AND SCRUBBERS) AND TWO-
    STAGE WET SCRUBBING STKATEGIES (SCRUBBER-ABSORBERS) FOR THE
    REMOVAL OF PARTICULATES AND SULFUR DIOXIDE.  A FINAL DECISION WILL
    BE ANNOUNCED BY THE UTILITY SHORTLY.
I.D. NUMBER   58
HINNKOTA POWER COOPERATIVE
MILTON R. YOUNG NO. 2
  t50  MW - NEW
LIGNITE - 6.500 BTu. 0.755 S
ADL/COMBUSTION EQUIP ASSOCIATE
LIME/ALKALINE FLYASH SCRUBBING
STARTUP   8/77
    THE CONTRACT FOR THIS LIME/ALKALINE FLYASH SCRUBBING SYSTEM HAS BEEN
    AWARDED TO ADL/COMBUSTION EQUIPMENT ASSOCIATES. THE EMISSION CONTROL
    SYSTEM FOR THIS UNIT CONSISTS OF A HIGH-EFFICIENCY ESP UPSTREAM OF TWO
    SPRAY TOWERS. DESIGN PARTICULATE ANU SULFUR DIOXIDE REMOVAL EFFICIENCIES
    ARE 99.6 AND 75 PERCENT.RESPECTIVELY. SITE PREPARATION AND FOUNDATION
    WORK HAS BEEN COMPLETED. ALL EQUIPMENT FABRICATION HAS BEEN COMPLETED.
    EQUIPMENT ERECTION IS NOW IN PROGRESS.  ALL HVAC AND ELECTRICAL CONTRACTS
    FOR THE SCRUBBER AND ANCILLARY EQUIPMENT HAVE BEEN AWARDED.
I.D. NUMBER   59
MONTANA POWER CO.
COLSTRIP NO 1
  360  MW - NEW
COAL   0.6 PERCENT SULFUR
ADL/COMBUSTION EQUIP ASSOCIATE
LIME/ALKALINE FLYASH SCRUBBING
STARTUP  10/75
    THE COLSTRIP PLANT IS A MINE MOUTH INSTALLATION. CONSTRUCTION ON THIS
    UNIT WAS COMPLETED BEHIND SCHEDULE. THE FGD SYSTEM STARTED UP IN LATE
    1975 AND PROCEEDED THROUGH A SHAKEDOWN AND DEBUGGING OPERATION PHASE. THE
    UNIT HAS BEEN OPERATING AT FULL COMMERCIAL CAPACITY.  THE SCRUBBING
    SYSTEM DESIGN INCORPORATES THE VENTURI WET SCRUBBERS FOR PARTICULATE
    AND SULFUR DIOXIDE REMOVAL.  FLUE GAS CANNOT BE BYPASSED AROUND THE
    SCRUBBING SYSTEM.  INFORMATION AND OPERATING DATA WERE NOT
    AVAILABLE BY THE UTILITY DURING THE REPORT PERIOD.
I.D. NUMBER   60
MONTANA POWER CO.
COLSTRIP NO 2
  360  MW - NEW
COAL   0.6 PERCENT SULFUR
ADL/COMBUSTION EOUjp ASSOCIATE
LIME/ALKALINE FLYASH SCRUBBING
STARTUP   7/76
    THE COLSTRIP PLANT IS A MINE MOUTH FACILITY. CONSTRUCTION OF THE FGD
    SYSTEM HAS BEEN COMPLETED. TURBINE KOLL AND SYSTEM CHECKOUT HAVE BEEN
    COMPLETED. INITIAL OPERATION OF THE SCRUBBING SYSTEM COMMENCED IN
    JULY 1976. THIS UNIT IS IDENTICAL TO THE NO.l SYSTEM DESIGN IN THAT
    THREE SCRUBBER MODULES ARE INSTALLED FOR PARTICULATE AND SULFUR DIOXIDE
    REMOVAL. FLUE GAS CONNOT BE BY-PASSED AROUND THE SCRUBBING SYSTEM.
    INFORMATION AND OPERATING DATA WERE NOT MADE AVAILABLE BY THE UTILITY
    DURING THE REPORT PERIOD,
                                                                22
                                                               PEDCO  ENVIRONMENTAL

-------
 COMPANY

 POWER STATION
           TABLE 2
STATUS OF F60 SYSTEMS DURING
       12/76

CURRENT MONTH
I.D. NUMBER   61
MONTANA POWER CO.
COLSTRIP NO.3'
  700  MW - NEW
COAL  0.7 PERCENT SULFUR
AOL/COMBUSTION EQUIP ASSOCIATE
LIME/ALKALINE FLYASH SCRUBBING
STARTUP   7/SO
    THE UTILITY ANNOUNCED DURING THE REPORT PERIOD THAT A CONTRACT FOR
    THE INSTALLATION OF TWO ADDITIONAL LIME/ALKALINE FLYASH SCRUBBING
    SYSTEMS HAS BEEN AWARDED TO AD LITTLE/COMBUSTION EOUlPfiENT ASSOCIATES.
    THESE SYSTEMS WILL BE INSTALLED ON UNITS NOS.  3 AND H OF THE COLSTRIP
    POWER STATION. COLSTRIP UNITS 1 AND 2 ARE BOTH EQUIPPED WITH OPERATIONAL
    LIME/ALKALINE FLYASH SCRUBBING SYSTEMS FOR THE REMOVAL OF PARTICULATES
    AND SULFUR DIOXIDE. ENGINEERING WORK FOrt THE NEW SYSTEMS IS NOW UNDERWAY.
    THIS CONTRACT IS EXPECTED TO EXCEED $50 MM.
I.D. NUMBER   62
MONTANA POWER CO.
COLSTRIP N0.<»
  700  MW - MEW
COAL  0.7 PERCENT SULFUR
ADL/COMBUSTIO.M EQUIP ASSOCIATE
LIME/ALKALINE FLYASH SCRUBBING
STARTUP   7/61
    THE UTILITY ANNOUNCED DURING THE REPORT PERIOD THAT A CONTRACT FOR
    THE INSTALLATION OF TWO ADDITIONAL LIME/ALKALINE FUYASH SCRUBBING
    SYSTEMS HAS BEEN AWAHULD TO AD LITTLE/COMBUSTION EQUIPMENT ASSOCIATES.
    THESE SYSTEMS WILL BE INSTALLED ON UNITS NOS. 3 AND "» OF THE COLSTRIP
    POwER STATION. COLSTRIP UNITS 1 AND 2 ARE BOTH EQUIPPED WITH OPERATIONAL
    LIME/ALKALINE FLYASH SCRUBBING SYSTEMS FOR THE REMOVAL OF PARTICULATES
    AND SULFUR DIOXIDE. ENGINEERING WORK FOR THE NEW SYSTEMS IS NOW UNDERWAY.
    THIS CONTRACT IS EXPECTED TO EXCEED $50 MM.
I.D. NUMBER   63
NEVADA POWER
HARRY ALLEN STATION NO. 1
  500  MW - NEW
COAL
NOT SELECTED
HOT SELECTED
STARTUP
    CONSIDERING HOT SIDE ESP IN CONJUNCTION WITH AN FGD SYSTEM.  SPECIFICA-
    TIONS HAVE NOT YET BEEN PREPARED.
I.D. NUMBER   6t
NEVADA POWER
HARRY ALLEN STATION NO.  2
  500  MW - NEW
COAL
NOT SELECTED
NOT SELECTED
STARTUP   6/BH
    CONSIDERING HOT SIDE ESP IN CONJUNCTION WITH AN FGD SYSTEM.  SPECIFICA-
    TIONS HAVE NOT YET BEEN PREPARED.
I.D. NUMBER    65
NEVADA POWER
HARRY ALLEN STATION  NO.  3
  500  MW  - NEW
COAL
NOT SELECTED
NOT SELECTED
STARTUP    6/85
    CONSIDERING HOT SIDE ESP IN CONJUNCTION WITH AN FGD SYSTEM.  SPECIFICA-
    TIONS HAVE NOT YET BEEN PREPARED.
                                                                                                  PEOCO ENVIRONMENTAL

-------
  COMPANY

  POWER STATION
                                             TABLE 2
                                  STATUS- OF FGD SYSTEMS DURING
                          12/76

                   CURRENT MONTH
' 1.0.  NUMBER   66
 NEVADA POWER
 HARRY ALLEN STATION NO.
   500  Mh - NEW
 COAL
 NOT SELECTED
 NOT SELECTED
 STARTUP   6/86
                                      CONSIDERING HOT SIDE ESP IN CONJUNCTION WITH AN FGD  SYSTEM.  SPECIFICA-
                                      TIONS HAVE NOT YET BEEN PREPARED.
 1.0.  NUMBER   67
 NEVADA POWER
 REID GARDNER NO 1
   125  HW - RETROFIT
 COAL   0.5- 1.0 PERCENT SULFUR
 AOL/COMBUSTION EQUIP ASSOCIATE
 SODIUM CAKBOMATE SCRUBBING
 STARTUP
                                       REFER  TO  THE BACKGROUND INFORMATION  SECTION  IN TABLE  3 OF THIS REPORT.
                                       THIS SODIUM CARBONATE-BASED  (TRONA)  SCRUBBING SYSTEM  CONSISTS OF  ONE
                                       MODULE CONTAINING  A  TWIN VARIABLE-THROAT  VENTURI  SCRUBBER FOLLOWED  BY A
                                       SINGLE-STAGE PERFORATED-PLATE  WASHING  TOWER.  THE SCRUBBING  TRAIN
                                       WAS FIRST PLACED  IN  OPERATION  IN  APRIL 197H.  THE SYSTEM WAS IN SERVICE
                                       THROUGHOUT THE  REPORT  PERIOD.  LOGGING  SERVICE TIMES OF 508 HOURS  AND
                                       599 HOURS FOR THE  MONTHS OF  NOVEMBER AND  DECEMBER. RESPECTIVELY.
               68
1I.D.  NUMbER
 NEVADA POWER
 REID  GARDNER NO 2
   125  Mw  -  RETROFIT
 COAL    0.5-  1.0 PERCENT SULFUR
 ADL/COMBUSTION EQUIP ASSOCIATE
 SODIUM CAKBUNATE SCRUBBING
 STARTUP   H/7H
REFER TO THE BACKGROUND INFORMATION SECTION IN TABLE 3 OF THIS REPORT.
THIS SODIUM CARBONATE-BASED (TRONA) SCRUBBING SYSTEM CONSISTS OF ONE
MODULE CONTAINING A TWIN VARIABLE-THROAT VENTURI SCRUBBER FOLLOWED BY A
SINGLE-STAGE PERFORATED-PLATE WASHING TOWER.  THE SCRUBBING TRAIN WAS
FIRST PLACED IN THE GAS PATH IN APRIL 1974.  SYSTEM OPERATION DURING THE
REPOKT PERIOD WAS INTERMITTENT BECAUSE OF SCRUBBER AND BOILER-RELATED
PROBLEMS.
'I.D. NUMBER   69
 NEVADA POWER
 REID GARDNER NO 5
  1 125  Kw - NEW
 COAL   0.5- 1.0 PERCENT SULFUR
 ADL/COMBUSTION EQUIP ASSOCIATE
 SODIUM CARBONATE SCRUBBING
 STARTUP   7/76
                                       REFEK TO THE BACKGROUND INFORMATION SECTION IN TABLE 3 OF THIS REPORT.
                                       THIS UNIT IS A NEW COAL-FIRED BOILER THAT IS EQUIPPED WITH SODIUM
                                       CAKBONATE-BASED(TRONA)SCRUBBING SYSTEM WHICH INCORPORATES A TWIN
                                       VARIABLE-THROAT VENTURI SCRUBBER FOLLOWED BY A SINGLE-STAGE PERFORATED-
                                       PLATE WASHING TOWEK FOR THE CONTROL OF PARTICULATES AND SULFUR
                                       DIOXIDE.  THE BOILER COMMENCED OPERATIONS IN APRIL 1976 AND THE
                                       SCRUBBER WAS PLACED IN SERVICE THREE MONTHS LATER.  THE SYSTEM
                                       WAS IN SERVICE THROUGHOUT THE REPORT PERIOD.
'I.D. NUMBER   70
 NEVADA POWER
 REID GARDNER NO H
   125  MW - NEW
• COAL   0-5- l.Q PERCENT SULFUR
 ADL/COMBUSTION EQUIP ASSOCIATE
 SODIUM CARBONATE SCRUBBING
 STARTUP   O/ 0
                                       NEVADA POWER COMPANY HAS SIGNED A LETTER OF INTENT WITH COMBUSTION EQUIP-
                                       MENT ASSOCIATES FOR THL CONSTRUCTION OF AN FGD SYSTEM ON REID GARDNER NO.
                                       «».   HOWEVER. CONSTRUCTION OF THE BOILER HAS BEEN INDEFINITELY POSTPONED.
                                                                                                   PCDtO ,

-------
 COMPANY

 POWER STATION
           TABLE 2
STATUS OF FGO SYSTEMS DURING
       12/76

CURRENT MONTH
1.0. NUMBER   71
NEVADA POWER
WARNER VALLEY STATION NO. 1
  250  MU - NEW
COAL
NOT SELECTED
NOT SELECTED
STARTUP   6/62
    SPECIFICATIONS ARE BEING PREPARED FOR A SCRUBBING SYSTEM.
I.D. NUMBER   72
NEVADA POWER
WARNER VALLEY STATION NO.
  250  MW - NEW
COAL
NOT SELECTED
NOT SELECTED
STARTUP   6/83
    SPECIFICATIONS ARE BEING PREPARED FOR A SCRUBBING SYSTEM.
I.D. NUMBER   73
NEW ENGLAND ELEC SYSTEM
BRAYTON POINT NO.3
  650  MW - RETROFIT
COAL 3.0 PERCENT SULFUR
NOT SELECTED
REGENERABLE NOT SELECTED
STARTUP   O/ 0
     THE UTILITY IS CURRENTLY INVESTIGATING VARIOUS ADVANCED REGENERABLE
     FLUE GAS DESULFURIZATION SYSTEMS WHICH OFFER A BREAKTHROUGH IN
     OPERATING COSTS AND PRODUCE ELEMENTAL SULFUR AS AN END
     PRODUCT.  THE UTILITY IS CURRENTLY INVOLVED IN BENCH AND LABORATORY
     SCALE INVESTIGATIONS OF SULFUR RECOVERY.  THE NO. 3 UNIT IS CURRENTLY
     OPERATIONAL. FIRING LOW SULFUR FUEL OIL.
I.D. NUMBER   7*t
NIAGARA MOHAWK POWER COOP.
CHARLES K. HUNTLEY NO. 6
  100  MW - RETROFIT
COAL 2.5-«u5 PERCENT SULFUR
ATOMICS INTERNATIONAL
AQUEOUS CARBONATE SCRUBBING
STARTUP   6/78
    THE EMPIRE STATE ELECTRIC ENERGY RESEARCH CORP.
    BY THE EPA TO NEGOTIATE FOR THE INSTALLATION OF
    SCRUBBING SYSTEM UTILIZING SULFUR RECOVERY. THE
    SITE IS THE C.R. HUNTLEY STATION OF THE NIAGRA
    NEAR BUFFALO, NEW YORK. THE PROCESS BEING GIVEN
    THE AQUEOUS CABONATE SCRUBBING PROCESS OFFERED
    THE DESIGN COAL SPECIFICATIONS CALL FOR 2.5 TO
    TO BE BUhNED WITH AN S02 REMOVAL EFFICIENCY OF
                             HAS BEEN GIVEN PERMISSION
                             A 100-MW DEMONSTRATION
                             DESIGNATED INSTALLATION
                            MOHAWK POWER COOP LOCATED
                             PRIMARY CONSIDERATION IS
                            BY ATOMICS INTERNATIONAL.
                            «*.5 PERCENT SULFUR COAL
                            90 PERCENT OR 200 PPM.
I.D. NUMBER   75
NORTHERN INDIANA PUB SERVICE
BAILLY NO. 7
  190  MW - RETROFIT
COAL 3 PERCENT SULFUR
NOT SELECTED
NOT SELECTED
STARTUP   0/0
    CONSIDERING A LIME OR LIMESTONE SCRUBBING UNIT.  ALSO WAITING FOR PER-
    FORMANCE OF WELLMAfc LORD/ALLIED CHEMICAL UNIT UNDER CONSTRUCTION AT THEIR
    D.N.MITCHELL NO.11 UNIT. LOW SULFUR COAL MAY BE EMPLOYED TO COMPLY WITH
    S02 EMISSION REGULATIONS.
                                                                25
                                                                PEDCO ENVIRONMENTAL

-------
 COMPANY

 POWER STATION
           TABLE 2
STATUS OF F60 SYSTEMS DURING  12/76

                       CURRENT MONTH
I.D. NUMBER   76
NORTHERN INDIANA PUB SERVICE
BAILLY NO. 8
  400  MW - RETROFIT
COAL 3 PERCENT SULFUR
NOT SELECTED
NOT SELECTED
STARTUP   O/ 0
    CONSIDERING A LIME OR LIMESTONE SCRUBBING UNIT.  ALSO WAITING FOR PERFOR-
    MANCE OF WELLMAN LORD/ALLIED CHEMICAL UNIT UNDER CONSTRUCTION AT THEIR
    0. H. MITCHELL NO. 11 UNIT.  LOW SULFUR COAL MAY BE BURNED TO COMPLY WITH
    S02 EMISSION REGULATIONS.
I.D. NUMBER   77
NORTHERN INDIANA PUBLIC SERVIC
D.H. MITCHELL NO.ll
  115  MW - RETROFIT
COAL   3.2- 3.5 PERCENT SULFUR
DAVY POWERGAS/ALLIEO CHEMICAL
WELLMAN LORD/ALLIED CHEMICAL
STARTUP   0/77
    THIS FGO SYSTEM  IS AN INTEGRATION OF THE WELLMAN-LORO S02 RECOVERY PRO-
    CESS OF DAVY POWE.RGAS AND ALLIED CHEMICAL'S S02 TO SULFUR REDUCTION
    PROCESS. DAVY POWERGAS  IS THE ENGINEER AND CONSTRUCTOR OF THE FGD
    FACILITY AND ALLIED CHEMICAL IS THE SYSTEM OPERATOR AND PRODUCT MARKETERt
    AT THE PRESENT TIME. INITIATIATION OF OPERATIONS OF THE S02 RECOVERY
    SYSTEM HAVE BEEN OE-LAYfcO BY BOILER UNAVAILABILITY.  START-UP OF SYSTEM
    OPERATIONS IS INDEFINITE.  ALL PROGRAM PARTICIPANTS ARE ANALYZING
    VARIOUS STRATEGIES TO MINIMIZE THE LENGTH OF THE DELAY PERIOD.
I.D. NUMBER   78
NORTHERN STATES POWER CO.
SHERBURNE COUNTY STATION NO.l
  710  Mfci - NEW
COAL 0.8 PERCENT SULFUR
COMBUSTION ENGINEERING
LIMESTONE SCRUBBING
STARTUP   3/76
     REFEK TO  THE  BACKGROUND  INFORMATION  SECTION  IN TABLE  3  OF  THIS REPORT.
     A PRELIMINARY  WATLR/AIR  SYSTEM CHECKOUT  WAS  SUCCESSFULLY COMPLETED  BY
     THE  UTILITY AND  INITIAL  OPERATIONS COMMENCED ON  MARCH 16,  1976.  FULL
     COMMERCIAL OPERATION OF  THE  SYSTEM BEGAN ON  MAY  1.  1976. THE  SCRUBBING
     SYSTEM  FOR THIS  UNIT CONSISTS OF  12  MODULES. EACH  SCRUBBING MODULE
     INCORPORATES  A VENTURI-ROD SECTION AND A MARBLE  BED ABSORBER  FOR PAR-
     TICULATE  AND  SULFUR DIOXIDE  REMOVAL.  SYSTEM  DESIGN CALLS FOR  11  MODULES
     TO BE IN  OPERATION FOR FULL  LOAD  CAPACITY.
 I.D. NUMBER   79
 NORTHERN STATES POWER CO.
 SHERBURNE COUNTY STATION NO.2
. 680  MW - NEW
 COAL 0.8 PERCENT SuLFUR
 COMBUSTION ENGINEERING
 LIMESTONE SCRUBBING
 STARTUP   5/77
     THL  CONSTRUCTION  Of-  THIS  NEW  POWER-GENERATING  UNIT IS VIRTUALLY  COMPLETE.
     THE  EARLY  STAGES  OF  SYSTEM CHECKOUT  IS NOW  IN  PROGRESS.   BOILOUT AND
     STLAM BLOWOUT  HAVE BEEN COMPLETED.   GAS HAS BEEN PASSED  THROUGH  THE
     SCKUiiBER MODULES. TUKBINE KOLL HAS  BEEN SCHEDULED FOR THE LAST  WEEK
     IN JANUARY 1977.   THE DESIGN  OF THE  EMISSION CONTROL SYSTEM FOR  THIS UNIT
     is IDENTICAL TO THE  SYSTLM NOW OPERATIONAL  ON  THE NO. i  UNIT.  THE SYSTEM
     DOES NOT  INCLUDE  FLUE GAS BY-PASS CAPABILITY.  NECESSITATING THE
     SIMULTANEOUS START-UP OF  BOTH THE BOILER AND SCRUBBING SYSTEM.
I.D. NUMBER   80
NORTHERN STATES POWER CO.
SHERBURNE COUNTY STATION NO.3
  860  MW - NEW
COAL 0.8 PERCENT SULFUR
NOT SELECTED
NOT SELECTED
STARTUP   5/81
     NSP  HAS  ANNOUNCED THAT  TWO  ADDITIONAL COAL-FIRED POWER.GENERATING UNITS
     ARE  SCHEDULED TO BE  INSTALLED AT THEIR SHERBURNE COUNTY GENERATING
     STATION  IN  BECKER, MINNESOTA. COMMERCIAL OPERATION DATES ARE NOW
     SCHEDULED FOR MAY 1961  AND  MAY 1983.  EACH UNIT IS NOMINALLY RATED AT
     860  MW.  THE BOILERS  WILL  BE DESIGNED  TO FIRE  MONTANA LOW-SULFUR SUB-
     BITUMINOUS  COAL  WITH A  HEAT CONTENT OF 6300 BTU/LB AND ASH AND SULFUR
     CONTENTS OF 9.0  AMU  0.6 PERCENT,  RESPECTIVELY. THE UTILITY IS CONSIDERING
     TWO-STAGE SCRUBBERS  FOR THE CONTROL OF PARTICULATES AND SULFUR DIOXIDE.
                                                                                                  PEOCO ENVIRONMENTAL

-------
 COMPANY

 POWER STATION
           TABLE 2
STATUS OF F60 SYSTEMS DURING  12/76

                       CURRENT MONTH
I.D. NUMBER   al
NORTHERN STATES POWER CO.
SHERbURNE COUNTY STATION N0.«»
  860  MM - NEW
:OAL o.s PERCENT SULFUR
MOT SELECTED
*OT SELECTED
STARTUP   5/83
    NSP HAS ANNOUNCED THAT TWO ADDITIONAL COAL-FIRED POWER-GENERATING UNITS
    ARE SCHEDULED TO BE INSTALLED AT THEIR SHERBURNE COUNTY GENERATING
    STATION IN BECKER, MINNESOTA. COMMERCIAL OPERATION DATES ARE NOW
    SCHEDULED FOR MAY 1981 AND MAY 1985. EACH UNIT IS NOMINALLY RATED AT
    860 MW. THE BOILERS WILL BE DESIGNED TO FIRE MONTANA LOW-SULFUR SUB-
    BITUMINOUS COAL WITH A HEAT CONTENT OF 8300 BTU/LB AND ASH AND SULFUR.
    CONTENTS OF 9.0 AND 0.6 PERCENT, RESPECTIVELY. THE UTILITY IS CONSIDERING
    TWO-STAGE SCRUBBERS FOR THE CONTROL OF PARTICULATES AND SULFUR DIOXIDE.
I.D. NUMBER   82
OTTER TAIL POWER COMPANY
COYOTE STATION NO.l
  HOO  MW - NEW
LIGNITE 0.9 PERCENT SULFUR
UOT SELECTED
NOT SELECTED
STARTUP   0/81
    THIS NEW COAL-FIRED STATION IS JOINTLY OWNED BY FIVE UTILITIES. OTTER
    TAIL POWER IS THL MAJOR OWNER AND CONSTRUCTOR. MONTANA-DAKOTA UTILITIES
    IS THE FACILITY OPERATOR. THIS PLANI4ED UNIT WILL FIRE LOW SULFUR LIGNITE
    FROM THE MERCER COUNTY AREA. THE UTILITY IS NOW INVESTIGATING VARIOUS
    EMISSION CONTROL STRATEGIES TO MEET PARTICULATE AND SULFUR DIOXIDE
    COOES. SULFUR DIOXIDE REMOVAL STRATEGIES BEING CONSIDERED AT THE PRESENT
    INCLUDE BOTH WET AND DRY REMOVAL PROCESSES.
:i.D. NUMbER   83
PACIFIC PUWER AND LIGHT CO.
JIM BRIDGER NO. *t
  509  MW - MEW
COAL 0.56 PERCENT SULFUR(AVG.)
UNIVERSAL OIL PRODUCTS
SODIUM CARBONATE SCRUBBING
STARTUP   9/79
    THE PACIFIC POWEK & LIGHT CO. AND  IDAHO POWER CO. HAVE ANNOUNCED THAT THE
    PLANS FOR AN EMISSION CONTROL STRATEGY FOR THEIR NEW POWER GENERATING
    UNIT AT THE JIM BRIDGER PLANT HAVE BEEN FINALIZED. UNIT NO.f WILL FIRE A
    LOW SULFUR  (0.56 PERCENT) SUBBITUMINOUS COAL AND HAS A NET RATING OF 509
    MW. PARTICULATES AND SULFUR DIOXIDE WILL BE CONTROLLED BY A ELECTROSTATIC
    PRECIPITATOR UPSTREAM OF A SODIUM-BASED WET SCRUBBING SYSTEM. THE FGD
    CONTRACT HAS BEEN AWARDED TO UOP FOR THREE ABSORPTION TRAINS DESIGNED TO
    REMOVE 91 PERCENT OF THE S02 TO MEET THE STRICT WYOMING EMISSION COOES.
7.D. NUMBER   84
PENNSYLVANIA POWER CO.
BRUCE MANSFIELD NO. 1
  835  MW - NEW
COAL <*.7 PERCENT SULFUR
C.HEMICO
LIME SCRUBBING
J.TARTUP   n/je>
    HEFER TO THE BACKGROUND INFORMATION SECTION IN TABLE 3 OF THIS REPORT.
    THIS EMISSION CONTROL SYSTEM IS CAPABLE OF REMOVING FLYASH AND S02 FROM
    3.35 MM ACFM OF FLUE GAS VIA WET LIME SCRUbBItJG. THE INITIAL SHAKEDOWN
    AND DEBUGGING PHASE OF OPERATION BEGAN FOR PART OF THE SYSTEM IN DECEMBER
    1975. FULL COMMERCIAL OPERATION COMMENCED IN APRIL 1976. TO DATE, ALL 6
    OF THE SCRUBBING TRAINS HAVE BEEN SUCCESSFULLY PUT INTO OPERATION.
    THE AVAILABILITY INDEX VALUE FOR THE ENTIRE SCRUBBING SYSTEM HAS
    BEEN IN THE MID 90 PERCENT RANGE SINCE COMMERCIAL START-UP.
I.D. NUMBER   85
PENNSYLVANIA POWER CO.
tRUCE MANSFIELD NO. 2
  835  MW - NEW
COAL H.7 PERCENT SULFUR
cHEMico
LIME SCRUBBING
STARTUP   H/77
    THE FGO SYSTEM FOR THIS INSTALLATION WILL BE A CHEMICO WET LIME SCRUBBING
    SYSTEM CAPABLE OF REMOVING PARTICULATE MATTER AND S02 FROM THE FLUE GAS.
    THIS SYSTEM IS CURRENTLY UNDER CONSTRUCTION. LONG DELAYS HAVE BEEN EN-
    COUNTERED IN MATERIAL DELIVERIES. THE FGD SYSTEM STAKTUP DATE IS NOW
    SCHEDULED FOR APRIL 1977. THE DESIGN, ARRANGEMENT AND OPERATION OF THIS
    SCRUBBING SYSTEM WILL BE IDENTICAL TO THE NO.l UNIT CURRENTLY OPERATIONAL
    AT THIS STATION
                                                                27
                                                                PEDCO ENVIRONMENTAL

-------
  COMPANY
  , • I   -I
  POWER  STATION
           TABLE: 2
STATUS OF F6D SYSTEMS DURING  12/76
                       CURRENT MONTH
 I.D.  NUMBER    86
'PENNSYLVANIA  POWER CO.
 BRUCE MANSFIELD NO.  3
   635  MW  - NEW
 COAL  H.7 PERCENT  SULFUR
 PULLMAN KELLOGG
 LIME  SCRUBBING
 STARTUP   H/79
    THE PULLMAN KELLOGG DIVISION OF PULLMAN INCORPORATED HAS BEEN
    AWARDED A CONTRACT IN EXCESS $50 MILLION BY THE CAPCO CONSORTIUM
    FOR THE INSTALLATION OF SULFUR DIOXIDE SCRUBBER ON THIS 035 MW COAL-
    FIREU POWER-GENERATING UNIT.  THE EMISSION CONTROL SYSTEM FOR THIS
    UNIT WILL CONSIST OF ESP«S FOR PARTICULATE CONTROL UPSTREAM OF
    5 WEIK HORIZONTAL CROSSFLOW WET SCRUBBING MODULES EMPLOYING A
    THIOSORBIC LIME SCRUBBING SOLUTION FOR THE REMOVAL OF SULFUR
    DIOXIDE.  CONSTRUCTION OF THE BOILER IS CURRENTLY IN PROGRESS.
 1.0.  NUMBER    87
'PHILADELPHIA ELECTRIC  CO.
 CROfiBY
   150  MW -  RETROFIT
 COAL    2-<» PERCENT SULFUR
 UNITED ENGINEERS  / PECO
 MAGNESIUM OXIDE SCRUBBING
 STARTUP   6/60
    THt. UTILITY PLANS TO RETROFIT ONE OF THE TWO BOILERS AT CROMBY WITH  AN
    FGO SYSTEM. HOUEVEK, A FINAL DECISION HAS NOT BEEN MADE.  THE PROCESS
    BEING GIVEN PRIME CONSIDERATION IS MAGNESIUM OXIDE SCRUBBING DESIGNED
    JOINTLY BY UNITED ENGINEERS AND PHILADELPHIA ELECTRIC.  ENGINEERING
    DESIGN WORK IS SCHEDULED TO COMMENCE IN 1977.  TENATIVE FGD SYSTEM
    START-UP  IS SCHEDULED FOR JUNE I960.
 I.D. NUMBER   86
 PHILADELPHIA ELECTRIC CO.
 EODYSTONE NO 1A
   120  MW - RETROFIT
 COAL   2.5 PERCENT SULFUR
 UNITED ENGINEERS / PECO
 MAGNESIUM OXIDE SCRUBBING
 STARTUP   9/75
    REFER TO  THE  BACKGROUND  INFORMATION SECTION IN TABLE 3 OF THIS REPORT.
    THE S02 SCRUBBING OPERATIONS HAVE BEEN TEMPORARILY DISCONTINUED AT THIS
    STATION BECAUSE  THE REGENERATION FACILITY AT THE OLIN CHEMICAL SULpURIC
    ACID PLANT  HAS PERMANENTLY CEASED OPERATIONS.  THE UTILITY  IS NOW RELO-
    CATING THE  REGENERATION  FACILITY TO THE ESSEX CHEMICAL PLANT LOCATED
    IN NEWARK,  NEW JERSEY. RESUMPTION OF S02 SCRUBBING OPERATIONS IS NOW
    SCHEDULED FOR MAY OF  1977.  TO DATE* THE MAGNESIUM OXIDE SCRUBBING UNIT
    HAS BEEN  IN SERVICE FOR  ONLY A SHORT PERIOD OF TIME DURING  LATE 1975.
 I.D. NUMBER   89
 PHILADELPHIA ELECTRIC CO.
 EDDYSTONE NO IB
   240  MW - RETROFIT
 COAL 2.5 PERCENT SULFUR
 UNITED ENGINEERS / PECO
 MAGNESIUM OXIDE SCRUBBING
 STARTUP   t>/80
     THE  INSTALLATION  OF  S02  SCRUBBERS  ON  THE  BALANCE  OF  THE  FLUE  GAS FROM
     THIS UNIT  WILL  FOLLOW  PENDING  THE  OUTCOME OF  THE  PERFORMANCE  OF THE
     SCRUBBING  UNIT  WHICH HAS BEEN  INSTALLED AND INTERMITTENTLY  OPERATIONAL
     ON THE  EODYSTONE  fJO.l  UNIT.  CURRENTLY. 3  WET  PARTICULATE SCRUBBERS ARE
     IN SERVICE ON  THIS UNIT.  THE  UTILITY REPORTS THAT'PROBLEMS WITH THE
     SCRUBBER BOOSTER  FANS  HAVE HOPEFULLY  BEEN SOLVED  AND WILL BE  RETURNED
     TO SERVICE WHEN THE  UNIT RETURNS TO OPERATION FOLLOWING  AN  EXTENDED
     SCHEDULED  SHUTDOWN FOR OVERHAUL AND REPAIR.
 I.D. NUMBER   90
 PHILADELPHIA ELECTRIC CO.
 EDDYSTONE NO. 2
   336  MW - RETROFIT
 COAL 2.«t PERCENT SULFUR
 UNITED ENGINEERS / PECO
 MAGNESIUM OXIDE SCRUBBING
 STARTUP   6/60
     THE UTILITY  IS  AWAITING  PERFORMANCE  RESULTS  FROM THE EXISTING  MAGOx
     SCRUBBER  INSTALLED  Ofv  UNIT  UO.l  AT THIS  STATION  BEFORE PROCEEDING
     WITH  THE  DESIGN OF  AN  FGU SYSTEM FOR THIS  COAL-FIRED BOILER. THE PROCESS
     BEING  GIVEN  PRIME CONSIDERATION  IS MAGNESIUM OXIDE  SCRUBBING DESIGNED
     JOINTLY BY UNITED ENGINEERS AND  PHILADELPHIA ELECTRIC. ENGINEERING
     DESIGN WORK  IS  SCHEDULED TO COMMENCE IN  1977.  TENATIVE FGD SYSTEM
     START-UP  IS  SCHEDULED  FOR JUNE 1980.
                                                                 28
                                                                PEDCO ENVIRONMENTAL

-------
 January 31, 1977
                               PEDCo- ENVIRONMENTAL
                                    SUITE 13 • ATKINSON SQUARE
                                          CINCINNATI. OHIO 45246
                                                    513 /771-433O
 Enclosed is a copy of the November-December report on  the
 Status of Flue Gas Desulfurization Systems in the United
 States.  This report is prepared  every other month by  PEDCo-
 Environmental, Inc., under a  contract to the Industrial
 Environmental Research Laboratory/RTF and the Division of
 Stationary Source Enforcement of  the U.S. Environmental
 Protection Agency.  Table I,  listed below, summarizes  the
 current status of these systems.

                            Table  I

              NUMBER AND TOTAL MW  OF FGD SYSTEMS
Status
Operational
Under construction
Planning
Contract awarded
Letter of intent
Requesting/evaluating bids
Considering only FGD systems
TOTAL
No. of
units
30
31

20
2
4
37
124
MW
6,476
13,309

9,981
365
2,327
16,726
49,184
Table II, gives  the  categorized breakdown  for  FGD units,
comparing the December report totals with  those  of the
October report.

Table III summarizes the individual units  that changed
status during the  report period.
              BRANCH OFFICES
 Suite 110. Crown Canter
 Kansas City, Mo. 64108
Suite 107-B Profenlonal Village
  Chapel Hill, N.C. 27514

-------
                           Table II

              NUMBER AND TOTAL MW OF FGD SYSTEMS

       DECEMBER REPORT PERIOD VERSUS OCTOBER REPORT PERIOD
Status
Operational
Under constructio:
Planning
Total
November-December
1976
No. of
units
30
\ 31
63
124
MW
6,476
13,309
29,399
49,184
September-October
1976
No. of
units
30
24
67
121
MW
6,476
9,869
30,589
46,934
The performance of the operating systems is summarized in
Table IV.  Other activity highlights during the months of
November and December are outlined below:

Allegheny Power System reported that construction is under-
way at the utility's Pleasants1 Units No. 1 and 2, in Bell-
mont. West Virginia.  Construction is currently in the
foundation phase and a 1000-foot stack shell has been erected,
The flue gas from these two 625-MW units will be scrubbed by
Babcock and Wilcox spray towers utilizing a recirculating
thiosorbic lime slurry.  APS and Babcock and Wilcox are
currently in the process of analyzing data from a recently
completed 5000-acfm pilot study which simulated conditions
that will apply to full-scale installations.  This data will
be utilized to ascertain optimal scrubber operating condi-
tions.  Pleasants1 Units No. 1 and 2 are scheduled for
start-up in March 1979, and March 1980, respectively.

Arizona Public Service reported the following items in
connection with the utility's FGD installations:

     Cholla No. 1 remained in service throughout the report
     period.   The average system reliability index values
     for the months of November and December were 99.7 and
     99.7 percent, respectively.

-------
     Construction of Cholla No. 2 is still in progress and
     on schedule.  Start-up is scheduled for June 1978.

     The experimental horizontal module at the Four Corners
     plant operated during the month of November, the test
     program was concluded December 6, 1976, and the scrubber
     unit has been dismantled.  A summary report on the test
     results is expected in March 1977.

Basin Electric Power Cooperative reported that it has award-
ed a contract to Research-Cottrell for limestone scrubbing
systems at the utility's Missouri Basin Units No. 1 and 2,
in Wheatland, Wyoming.  Both of these 550-MW units will fire
low-sulfur western coal, with a sulfur content of 0.8 per-
cent.  Babcock and Wilcox will provide the pulverized-coal,
dry-bottom boilers.  These units are scheduled for start-up
in April and October of 1980.  The units will have to comply
with the Wyoming emissions regulation of 0.2 Ib S02/MM Btu.

The Big Rivers Rural Electric Power Cooperative reported
that construction has begun on the Reid Steam Station, Unit
No. 2, a new 250-MW coal-fired unit, in Sebree, Kentucky.
The FGD system contract awarded to American Air Filter was
announced last report period.  Construction is currently in
the foundation-pouring phase with start-up scheduled for
late 1979.  The unit will be burning western Kentucky coal
with a sulfur content varying from 2.5 to 5.0 percent.

The Central Illinois Light Co. announced that scrubbing
operations have been temporarily terminated at the first of
four limestone scrubbing modules scheduled for its Duck
Creek Station, Unit No. 1.  The Ventri-Sorber scrubber
module had been.operating intermittently since mid-summer of
1976, and it was reported that the primary problem has been
scale build-up in the mist eliminator.  The unit operated 16
days in October,  1 day in November,  and in December, Duck
Creek No. 1 was switched to low-sulfur eastern Kentucky
coal, with a sulfur content of 0.6 percent.  Scrubbing
operations will not be restarted until the remaining three
scrubbing modules, controlling emissions from 300-MW of
generating capacity, have been installed.  Start-up for
these three modules is scheduled for August 1, 1978.  The
clarifying system and ball mill, and the major part of the
instrumentation for these modules has been installed.

Columbus and Southern Ohio Electric Co. reported that a
major fire, causing 2.1 million dollars damage, occurred at
the utility's Conesville Station in the A-side module on
Unit No. 5.  All scrubber internals were destroyed and the

-------
utility estimates repairs to the module will last through
June 1977.  The Conesville Unit No. 5 has two scrubbing
modules, each capable of handling 60 percent of the flue gas
flow.  Air and water testing of the undamaged B-side module
are scheduled to commence in January 1977.  Construction has
not yet begun on the Conesville No. 6 Unit.  Scheduled
start-up date is January 1978.

Commonwealth Edison reported that both scrubbing trains at
Will County were in service during the months of October and
November.  The availability index values reported for the A-
side and B-side trains were 28 and 76 percent, respectively,
in October and 20 and 72 percent, respectively, in November.
Simultaneous module service time for the same months were 0
and 47 hours, respectively.  Because of the low volume of
sludge produced during November, accumulated sludge in the
recirculation ponds was retrieved, stabilized with lime and
fly ash and transported to the off-site disposal area.

The Detroit Edison Company reported that the St. Clair No. 6
SO2 scrubber demonstration program continued during the
report period.  The utility reported availability index
values of 80 and 51 percent for November and December,
respectively.  Solids build-up on the I.D. fan was removed
by sandblasting and a decision was made to complete modifi-
cations such as fan rebalancing and wash system redesign
after the S02 demonstration program is completed.  The
program is currently scheduled for completion by February
1977.  Following the completion of the sulfur dioxide re-
moval program, the scrubbing system will continue to operate
in the particulate-removal mode only.

Duquesne Light reported the following items in connection
with the utility's FGD installations:

     Elrama continued with flue gas from two boilers being
     treated by five single-stage scrubbing vessels.  Also,
     the utility is conducting an evaluation of rubber-lined
     recycle pumps which have been installed on one of the
     vessels.

     Phillips operation continued with Boilers No. 2 through
     6 coupled into the scrubbing system.  The No. 1 boiler
     remains shutdown.  The interim IUCS sludge stabiliza-
     tion facility was installed and started up in December.
     A contract with Dravo for the purchase of magnesium
     lime was finalized and the new lime will be added to
     the system when the third and final thickener is cou-
     pled into the system.

-------
General Motors reported that the double alkali scrubbing
system at the Chevrolet Parma Steam Plant was operational
during the report period.  The FGD system operability index
values for the months of November and December were 60 and
22 percent, respectively.  Two of the four available boilers
operated during the period.  During the latter part of
November and early December, the scrubber was taken off-line
to resolve solids deposition in the mix tank, effected by
the modification of some piping arrangements.  A year-end
plant shutdown December 23, further reduced operability,
because the local U.A.W. contract specifies that the scrub-
ber may only be operated by union personnel.

Chiyoda International reported that on November 1, Southern
Services finished its evaluation of the CT-101 FGD prototype
unit.  A report on the test program and its results will be
published in the spring of 1977.  Gulf Power is continuing
scrubber operations for an unspecified time period in 1977,
in order to accumulate more data.  The unit's availability
index values for the months of November and December were
99.5 and 99.6 percent, respectively.  Three short periods of
forced scrubber outage occurred as a result of very minor
problems.  In December, a demonstration was successfully
completed, using 125 tons of synthetic gypsum to make wall
board.

Indianapolis Power and Light Co. announced during the report
period that a new 530-MW, coal-fired power generating unit
is being planned for their Petersburg Generating Station..
This new unit will fire high sulfur bituminous coal with an
average heat content of 11,000 Btu/lb and ash and sulfur
contents of 10 percent and 3.5 percent, respectively.  The
utility is considering various scrubbing strategies for the
control of sulfur dioxide, giving primary considerations to
wet limestone scrubbing.  Commercial operation is scheduled
for April 1982.  The utility also reported that construction
is 50 percent completed at the Petersburg Unit no. 3, 530-MW
boiler and FGD system.  Initial electrical work has begun
and the rubber lining within the scrubber is currently being
installed.

The Kansas City Power and Light Co. reported the following
items concerning FGD at the utility's LaCygne and Hawthorn
Power Stations:

     The seven scrubbing modules controlling emissions from
     the 820-MW,  coal-fired LaCygne Unit No.  1 performed
     well during the report period, with average availa-
     bilities of 94 and 90 percent for the months of Novem-

-------
     her and December, respectively.  The utility reported
     that no major scrubber problems occurred during Novem-
     ber.  During December, module A experienced venturi
     recycle pump problems, and module C had the number of
     reheat bundles doubled from four to eight.

     Major modifications to the scrubbing systems installed
     on the No. 3 and No. 4 units of the Hawthorn Station
     are continuing.  The existing systems installed on each
     boiler include a limestone-injection and dual-module
     tail-end wet scrubbing system.  These systems are now
     being converted to lime-based tail-end wet scrubbing
     systems.  Operation of both systems during the report
     period was limited because of the ongoing modifica-
     tions.  The A-module on Unit No. 4 was in service
     during the month of November, logging an operability
     index value of 91 percent.  All modification work is
     expected to be completed during the first quarter of
     1977.

Kansas Power and Light Co. reported the following items con-
cerning FGD at the utility's Jeffrey and Lawrence Power Sta-
tions:

     Construction is progressing on schedule at the Jeffrey
     Power Generating Station, Units No. 1 and 2.  These two
     units will function as base-load units, each having a
     generating capacity of 680 MW.  Each unit will fire 250
     T/hr of low-sulfur coal, with a sulfur content of 0.3
     percent and a heating value of 8000 Btu/lb.  Jeffrey
     Units No. 1 and 2 are scheduled for start-up in June
     1978, and June 1979, respectively.

     The utility reported that Lawrence Power Station Units
     No. 4 and 5 are still in the process of being changed
     over from boiler limestone injection to wet scrubbing
     systems designed and installed by Combustion Engi-
     neering.  C-E will be demonstrating a fully-automated
     scrubbing system on the 400-MW No. 5 unit.  This sulfur
     dioxide control system will consist of two large scrub-
     bing modules, each handling 50 percent of the boiler
     flue gas.  On this unit, the foundation and structural
     steelwork are in, and some breeching has been installed.
     C-E is currently working out the logic circuitry for
     this fully-automated control system.  The No. 4 unit,
     rated at 125 MW, is near to a scrubber system start-up
     date.  Start-up was delayed by scheduled turbine over-
     haul work in the fourth quarter of 1976.  Units No. 4
     and 5 will fire 50 and 140 T/hr, respectively, of
     pulverized coal with a sulfur content of 0.5 percent
     sulfur and a heating value of 10,000 Btu/lb.

-------
Kentucky Utilities reported that the Green River FGD system
achieved operability index values of 100 and 99.6 percent
for the months of November and December, respectively.  The
scrubber system was by-passed during part of the December
period for a check of scrubber internals and replacement of
balls in the mobile bed contactor.

The Key West Utility Board reported modifications and re-
pairs to the scrubbing system at the Stock Island generating
plant were delayed because replacement parts had not yet
been delivered.  The utility is planning a test period for
the first half of 1977.  The FGD system will then be shut
down because it is not required to meet regulations.

Louisville Gas and Electric reported the following items in
regards to the utility's FGD installations:

     The utility reported that the Cane Run Unit No. 4
     scrubber system utilized carbide lime for scrubbing
     during the months of November and December.  The oper-
     ability index values were 95 and 90 percent, respec-
     tively.

     The construction of Cane Run Unit No. 5 is proceeding
     on schedule.  Total installed capital cost of the sys-
     tem is estimated to be 12 million dollars for the
     capacity.

     The EPA-subsidized scrubber/sludge characterization
     study at Paddy's Run No. 6 unit was operational during
     November and December with an availability index value
     of 99.5 percent for the two-month period.  The scrubber
     operated with carbide lime during the report period.
     The high-calcium virgin lime operation has been delayed
     until approximately March 1, 1977, because of the
     current emergency power situation.

Minnkota Power Cooperative reported that all additional
contracts for heating, ventilation, air conditioning, elec-
trical, and ancillary equipment for the Milton R. Young No.
2 FGD system have been awarded.  In addition, construction
is ongoing and the utility is currently anticipating that it
will be ready for FGD system testing when the new 450-MW
unit is started-up in May 1977.

-------
     Nevada  Power  reported  the  following  items  regarding  the
     utility's  FGD installations:

     Reid Gardner  No.  1  was in  service  throughout  the  report
     period.  The  system availability index  values for the
     months  of  November  and December wer  86.5 and  92.7
     percent, respectively.   One forced scrubber outage
     occurred during November because of  a screw conveyor
     failure, resulting  in  an inability to mix  the chemical
     absorbent. Two forced scrubber outages occurred  during
     December because of chemical depletion  and a  plugged
     sensing line, respectively.

     Reid Gardner  No.  2  demonstrated an availability index
     value of  52 percent during November.  During  a boiler
     outage  to  repair a  condenser tube  leak  and bottom ash
     nozzle,  the scrubber's guillotine  dampers  were badly
     damaged,  and  the scrubber  remained out  of  service
     during  the month of December.

     Reid Gardner  No.  3  was not in operation during the
     first half of November due to repairs of  leaks in the
     venturi scrubber box.   The system was restarted Novem-
     ber 19,  and experienced one further  forced outage
     during  the month, because  of a screw conveyor malfunc-
     tion, preventing chemical  mixing.   During  the month of
     December,  one minor scrubber outage  occurred, because
     of repairs to the I.D. fan expansion joint.   The avail-
     ability index values for the months  of  November and
     December were 28.5  and 99.1 percent, respectively.

Northern Indiana Public  Service Co. announced that during
the report period  the Mitchell  No. 11  unit was  brought down
for a scheduled annual boiler overhaul.  The demonstration
Wellman-Lord SC>2 recovery system was awaiting completion of
the overhaul for initiation of its first extended period of
operation in an integrated mode.  Boiler unavailability of
the Mitchell No. 11 unit has resulted in an indefinite
period of delay of the demonstration S02 recovery program.
All participants in the program are now considering and
analyzing various alternatives that can minimize the delay
of the S02 recovery system start-up.

Northern States Power reported the following items con-
cerning the utility's FGD activity:

     Sherburne No. 1 remained in  service throughout the
     period achieving total system availability index  values
     of 93.0 and  94.7 percent for the months of November and

-------
     December, respectively.  Modification to the duplex
     strainer system is continuing with work about one-third
     complete.  The utility is currently conducting a full-
     load evaluation study, analyzing system operation on 10
     scrubber modules in contrast to the designed 11 modules.

     Construction on Sherburne No. 2 is proceeding ahead of
     schedule, with turbine roll now scheduled for mid-Janu-
     ary.  The projected start-up date is now March 1, 1977.

     The utility is now officially considering FGD for both
     the No. 3 and No. 4 units at the Sherburne County
     Generating Station.  Bid request and evaluation will
     start shortly.  Each of these Babcock and Wilcox
     boilers will have a nominal 860-MW rating, and will
     fire a sub-bituminous coal with a heating value of 8300
     Btu/lb and sulfur and ash contents of 0.8 and 9.0,
     respectively.  Particulate and SC^ emissions for each
     unit will be controlled by a two-stage scrubbing de-
     sign, and the design specifications will call for NSPS
     performance  (though particulate control will be more
     complete, in order to comply with opacity require-
     ments) .  Units No. 3 and No. 4 are scheduled for start-
     up in May 1981, and May 1983, respectively.

The Pennsylvania Power Co. reported that the Bruce Mansfield
No. 1 scrubbing system was available 100 percent during the
report period.  Limited service time during the month of"
November was caused by boiler-related problems.

Philadelphia Electric Co. reported that the 150-MW Cromby
unit is scheduled for a retrofit FGD unit to start-up in
June 1980.  Engineering design work is scheduled to commence
in 1977.  The plant will be subject to emissions regulations
more stringent than Federal NSPS.  MgO scrubbing operations
at the utility's Eddystone No. 1 unit are scheduled for re-
start in May 1977.  The utility is completing the relocation
of regeneration facilities to the Essex Chemical Plant in
Newark, New Jersey.  The No. 1 power generating unit has
been out of service since late November because of modifica-
tions to the booster fans.  Start-up of Eddystone No. IB
scrubbing operations is now scheduled for June 1980.
Engineering design work for the Eddystone No. 2 scrubbing
system is scheduled to commence in 1977, with system start-
up scheduled for June 1980.

Research-Cottrell reported that the Bahco wet lime scrubbing
system installed at the Rickenbacker AFB in Columbus, Ohio
did not operate during November because of completion of

-------
repairs to the I.D. fan housing.  The system operated during
the entire month of December with S02 removal efficiency
varying from 85 to 90 percent.  Lime feed was regulated on a
manual basis because of a mulfunctioning slaker.  The new
stoker boiler has not yet been placed in commercial opera-
tion, primarily because of problems related to the particu-
larly severe weather conditions.

South Carolina Public Service reported that construction is
progressing on schedule at its Winyah No. 2 Power Station in
Georgetown, South Carolina.  This new, coal-fired, 280-MW
unit will fire 1 percent sulfur coal and SC>2 emissions will
be controlled by a Babcock and Wilcox limestone scrubbing
system.  Start-up is scheduled for May 1, 1977.

Southern Indiana Gas and Electric Co. announced that in
December it awarded a contract to FMC for the installation
of a double-alkali scrubbing system on A.B. Brown Unit No.
1, a new 250-MW coal-fired unit.  The sodium-calcium (soda
ash/lime) system will generate a filter cake which will be
disposed in a landfill.  The system is currently under
construction.  A contract for the upstream ESP has not yet
been awarded.  Full commercial operation is scheduled for
January 1979.

Springfield City Utilities reported that the 200-MW South-
west No. 1 unit in Springfield, Missouri, did not start-up
as scheduled in December 1976.  The delay has been caused
primarily by electrical wiring problems, and the boiler
operation has been undergoing problems in the combustion
control and coal-handling system.  The experimental sludge
disposal strategy consists of stabilization with cement and
transport to an on-site landfill.  Scheduled start-up date
is now projected for February 1977.

The Bechtel Corporation reported that experimental work is
continuing at the Shawnee TVA/EPA/Alkali Scrubbing Test
Facility.  From mid-October through early December an inten-
sive flue gas characterization testing program was conducted
on the venturi/spray tower system with lime slurry.  For the
remainder of December the venturi/spray tower system was
down for modifications for two-stage oxidation testing.
During November,  the TCA unit was operated with fly ash-
laden flue gas using lime slurry without added magnesium
oxide.  SC>2 removal was about 80 percent.  In late November,
fly ash-free limestone tests without magnesium oxide addi-
tion were begun on the TCA system.  At the same stoichiom-
etry, the pH of the fly ash free slurry was 8.2 to 8.3 as
compared with 8.0 in previous runs with fly ash.

-------
Utah Power and Light Co. announced that a contract has been
awarded to Chemico for the installation of a S02 control
system at its Emery Unit No. 1, in Emery County, Utah.  The
Chemico scrubbing system will be preceded by an upstream
Buell/Envirotech ESP for  primary particulate control.  S02
emissions from this 400-MW unit will be controlled by a wet
lime, open-water-loop scrubbing system, removing SC>2 with a
design efficiency of 80 percent.  Sludge will be mixed with
fly ash and disposed on-site.  Start-up is scheduled for
June 1978.  At the utility's Huntington Power Station,
equipment is now arriving and construction of the scrubbing
system will commence shortly.  System start-up is scheduled
for June 1977.

-------
                 TABLE III




            SUMMARY OF CHANGES




FGD STATUS REPORT, NOVEMBER-DECEMBER,  1976
FGD status report
10/31/76
Allegheny Power System
Pleasants No 4 i
Pleasants No. 2
Basin Electric Power Coop.
Missouri Basin No. 1
Missouri Basin No. 2
Big Rivers Rural Electric Coop.
Reid No. 2
Central Illinois Light Co.
Duck Creek No. IB
Indianapolis Power and Light Co.
Petersburg No. 4
Kansas Power and Light Co.
Jeffrey No. 1
Jeffrey No. 2
Northern States Power Co.
Sherburne No. 3
Sherburne No. 4
South Carolina Public Service
Co.
'•"inyah No. 2
Southern Indiana Gas and
Electric Co.
A.B. Brown No. 1
Utah Power and Light
E-.ery No. 1
12/31/76
Operational
No.
30




















30
MW
6,476




















6,476
Under
construction
No.
24

+1
+1



+1

+1



•H
+1



+1




31
MW
9,869

625
625



250

300



680
680



280




13,309
Contract
awarded
No.
23

-1
-1

-H
+1

-1

-1



-1
-1



-1

+ 1

-n
20
MW
11,671

625
625

550
550

250

300



680
680



280

250

400
9,981
Letter of
intent
No.
3



















-1
2
MW
765



















400
365
Requesting/
evaluating
bids
No.
7



-1
-1













-1


4
MW
3,677



550
550













230


2,327
Considering
FGD
No.
34









+1



+ 1
+1






37
MW
14,476









530



860
860






16,726
Total
No.
121




















124
MW
46,934




















49,184

-------
               TABLE  IV.   PERFORMANCE  OF OPERATIONAL  UNITS


                            DURING THE REPORT  PERIOD
Flint
Choi la
Four Corner*
Duck Creak 1A
Hill County 1
St. Clair
Elrarna
Phillip*
Parma
Scholi -
Chiyoda
Hawthorn 3
Hawthorn 4
La Cygn*
Lawrence 4
Lawrence 5
Green River
1*2
Stock I aland
Cane Run
Paaay ' • kun
Coletrlp 1
Colctrlp 2
Reid Gardner 1
Reid Gardner 2
Reid Gardner 3
Sherburne 1
Bruce
Mansfield 1
Eddy (tone 1A
valmont 5
Rickenbacker
Shawnee 10A
Shawnee 10B
Total (30)
PCD lyaten
deeign
capacity
111
1«0
100
167
163
510 .
410
32
23
140
100
•20
125
400
64
37
ITS
6*
360
360
125
125
125
710
835
120
50
20
10
10
6.459
PCD unit
on-line
during
period*
US
160
100
16T
163
200
37$
16
23

100
620


64

178
64


125
12S
125
710



20
10
10
3,671
No
information
for thia
period

















360
360




(35





1,355
Shut down
throughout
period




110
3$
16

140


12S
400

37









120
50



1,233
FGD ay a ten
avell-
ability(%)««



46
•0



s»


»4


100





8«
$2
99
93







pee.



SI



99


90


71





91

28
95







FGD ayatem
opara-
bility(t)**
Nov.


40




99

46



100

95
99


81
58
97
100







0*0.







99





97

90
99


96

•a
100







rco eyatem
reliability
(»)••
-HOT: —


41




99





98





84
51
99








D«c.







99





87





98

29








FGD syatem
utilization
(»)*•
NOV •


38




99





98.





71
50
97








her.







99





70





87

29








ThU category include* the flu* gaa capacity being handled by the FOO ayatern at leaat part of the tin* during the
report period.
The percent figure* Hated en average value* for all the ayaten ccrubblng train* during the period in question.

-------
 COMPANY

 POWER STATION
           TABLE 2
STATUS OF FGD SYSTEMS DURING  12/76

                       CURRENT MONTH
1.0. NUMBER   91
POTOMAC ELECTRIC & POWER
OlCKERSOfj NO.l
  190  MW - RETROFIT
COAL
CHEMICO
NOT SELECTED
STARTUP   0/78
    THE UTILITY HAS AWARDED A CONTRACT TO CHEMICO AIR POLLUTION FOR THE
    INSTALLATION OF A WET SCRUBBING SYSTEM ON THIS UNIT.  THE SCRUBBER
    CONSISTS OF A SINGLE MODULE DOUBLE VENTURI THROAT UNIT. THE FIRST
    VENTURI STAGE IS DESIGNED FOR REMOVAL OF PARTICULATE  MATTER ONLY. THE
    SECOND VENTURI STAGE WILL BE INSTALLED FOR FUTURE CONSIDERATIONS IF
    THE UTILITY ELECTS TO SCRUB SULFUR UIOXIDE. THE DESIGN ALLOWS CON-
    SIDERATION FOR EITHER A REGENERATIVE OR NON-REGENERATIVE FGD SYSTEM.
I.D. NUMBER   92
POTOMAC ELECTRIC & POWER
DICKEKSON NO.2
  190  MW - RETROFIT
COAL
CHEMICO
NOT SELECTED
STARTUP   0/78
    THE UTILITY HAS AWARDED A CONTRACT TO CHEMICO AIR POLLUTION FOR THE
    INSTALLATION OF A WET SCRUBBING SYSTEM ON THIS UNIT. THE SCRUBBER
    CONSISTS OF A SINGLE MODULE DOUBLE VENTURI THROAT UNIT. THE FIRST
    VENTURI STAGE IS DESIGNED FOR REMOVAL OF PARTICULATE MATTER ONLY. THE
    SECOND VENTURI STAGE WILL BE INSTALLED FOR FUTURE CONSIDERATIONS IF
    THE UTILITY ELECTS TO SCRUB SULFUR DIOXIDE. THE DESIGN ALLOWS CON-
    SIDERATION FOR EITHER A REGENERATIVE OR NON-REGENERATIVE FGD SYSTEM.
 1.0. NUMBER   93
 PUBLIC SERVICE CO OF  COLORADO
 VALMONT NO. 5
    so  MW - 'RETROFIT
 COAL  0.72 PERCENT SULFUR
 UOP / PUB SERVICE OF  COLORADO
 LIMESTONE SCRUBBING
 STARTUP  10/7f
    REFER TO BACKGROUND INFORMATION SECTION IN TABLE 3 OF THIS REPORT. THIS
    SYSTEM HAS BEEN OPERATIONAL SINCE NOVEMBER 19-74. THE FGD SYSTEM CURRENTLY
    OPERATIONAL AT THIS STATION IS AN EXPERIMENTAL UNITt ORIGINALLY DESIGNED
    BY UNIVERSAL OIL PRODUCTS FOR PARTICULATE REMOVAL ONLY. ONE OF THE TWO
    PARALLEL SCRUBBING MODULES WAS CONVERTED TO LIMESTONE SCRUBBING FOR
    EXPERIMENTAL PURPOSES ONLY.
 I.D. NUMBER   9f
 PUBLIC SERVICE CO OF NEW MEX.
 SAN JUAN NO. 1
  375  MW - NEW
 COAL   0.8 PERCENT SULFUR
 DAVY POWERGAS/ALHED CHEMICAL
 WELLMAN LORD/ALLIED CHEMICAL
 STARTUP   7/77
    THE CONSTRUCTION OF THIS SYSTEM IS NOW UNDERWAY. THIS FGD SYSTEM IS AN
    INTEGRATIOiM OF THE WELLMAN LORD S02 RECOVERY PROCESS OF DAVY POWERGAS
    AND ALLIED CHEMICAL'S S02 REDUCTION TO SULFUR PROCESS. DAVY POWERGAS IS
    THE DESIGN ENGINEERING FIRM.  STEARNS AND ROGER IS THE SYSTEM CONSTRUCTOR.
    THE UTILITY WILL BE THE SYSTEM OPERATORS. A HOT SIDE ELECTROSTATIC
    PRECIPITATOR WILL BE INSTALLED UPSTREAM OF THE SCRUBBING UNIT. FOUR
    ABSORBER TOWERS WILL BE INSTALLED FOR EACH UNIT. THREE WILL CARRY THE
    FULL LOAD. MOLTEN SULFUR WILL BE STORED ON THE PLANT SITE.
I.D. NUMBER   95
PUBLIC SERVICE CO OF NEW MEX.
SAN JUAN NO. 2
  340  MW - RETROFIT
COAL   0.8 PERCENT SULFUR
DAVY POWERGAS/ALLIED CHEMICAL
WELLMAN LORD/ALLIED CHEMICAL
STARTUP   7/77
    THE CONSTRUCTION OF THIS SYSTEM IS NOW UNDERWAY. THIS FGD SYSTEM IS AN
    INTEGRATION OF THE WELLMAN LORD S02 RECOVERY PROCESS OF DAVY POWERGAS
    ANU ALLIED CHEMICAL'S S02 REDUCTION TO SULFUR PROCESS. DAVY POWERGAS IS
    THE DESIGN ENGINEERING FIRM.  STEARNS AND ROGER IS THE SYSTEM CONSTRUCTOR.
    THE UTILITY WILL BE THE SYSTEM OPERATORS. A HOT SIDE ELECTROSTATIC
    PRECIPITATOR UlLL BE INSTALLED UPSTREAM OF THE SCRUBBING UNIT. FOUR
    ABSORBER TOWERS WILL BE INSTALLED FOR EACH UNIT. THREE MODULES WILL CARRY
    THE FULL LOAD. MOLTEN SULFUR  WILL BE STORED ON THE PLANT SITE.
                                                                29
                                                                PEOCO ENVIRONMENTAL

-------
 COMPANY

 POWER STATION
           TABLE 2
STATUS OF FGD SYSTEMS DURING  12/76

                       CURRENT MONTH
I.D. NUMBER   96
PUBLIC SERVICE CO OF NEW HEX,
SAN JUAN NO. 3
  500  MW - NEW
COAL 0.8 PERCENT SULFUR
NOT SELECTED
REGENERABLE NOT SELECTED
STARTUP   5/81
    THE UTILITY HAS PLACED A HOLD ON FURTHER ENGINEERING DESIGN WORK AT THE
    PRESENT TIME. THE PROJECTED START-UP DATE FOR BOTH UNITS 3 AND «» IS
    MAY 1981. THE KELLMAN LORD AND OTHEK SULFUR DIOXIDE RECOVERY PROCESSES
    ARE NOW UNDER CONSIDERATION BY THE UTILITY. AN ESP WILL BE PROVIDED
    UPSTREAM OF THE FGD SYSTEM FOR PRIMARY PARTICULATE CONTROL.
I.D. NUMBER   97
PUBLIC SERVICE CO OF NEW MEX,
SAN JUAN NO. 4
  500  MW - NEW
COAL 0.8 PERCENT SULFUR
NOT SELECTED
REGENERABLE NOT SELECTED
STARTUP   5/61
    THE UTILITY HAS PLACED A HOLD ON FURTHER ENGINEERING DESIGN WORK AT THE
    PRESENT TIME. THE PROJECTED START-UP DATE FOR BOTH UNITS 3 AND <* IS
    MAY 1981. THE WELLMAN LORD AND OTHER SULFUR DIOXIDE RECOVERY PROCESSES
    ARE NOW UNDER CONSIDERATION BY THE UTILITY. AN ESP WILL BE PROVIDED
    UPSTREAM OF THE FGO SYSTEM FOR PRIMARY PARTICULATE CONTROL.
I.D. NUMBER   98
PUBLIC SERVICE OF INDIANA
GIBSON NO. 3
  650  MW - NEW
COAL 3.3 PERCENT SULFUR
NOT SELECTED
NOT SELECTED
STARTUP   0/78
    THE UTILITY HAS COMPLETED THE EVALUATION OF BID SPECIFICATIONS
    SUBMITTED FOR FGD SYSTEMS FOR BOTH UNITS 3 AND <* AT THIS STATION.
    NO DECISION HAS YET BEEN MADE.
 I.D.  NUMBER    99
 PUBLIC  SERVICE: OF  INDIANA
 GIBSON  NO.  
-------
 COMPANY

 POWER STATION
                                             TABLE 2
                                  STATUS OF F6D SYSTEMS DURING  12/76

                                                         CURRENT MONTH
I.D. NUMBER  101
SALT RIVER PROJECT
CORONADO NO.l
  3bO  MW - NEW
COAL 1.0 PERCENT SULFUR (MAX)
PULLMAN KELLOGG
LIMESTONE SCRUBBING
STARTUP   H/T3
                                      THIS  NEW  UNIT  WILL BURN  LOW  SULFUR WESTERN COAL.  80 PERCENT OF THE
                                      GAS WILL  BE  SCRUBBED  TO  MEET SULFUR DIOXIDE EMISSION REGULATIONS.
                                      THE UTILITY  ANNOUNCED THAT A CONTRACT  HAS BEEN AWARDED TO PULLMAN/KELLOGG
                                      FOR THE INSTALLATION  OF  TWO  WEIR  HORIZONTAL CROSSFLOW SCRUBBING MODULES.
                                      THE SCRUBBING  REAGENT WILL BE LIMESTONE.   THE CONTRACT FOR THE ESP HAS
                                      BEEN  AWARDED TO JOY/WESTERN  PRECIPITATION DIVISION.  THE CONSULTING
                                      ENGINEERING  AND CONSTRUCTION FIRM IS BECHTEL.
I.D. NUMBER  102
SALT RIVER PROJECT
CORONADO NO.2
  350  MW - NEW
COAL 1.0 PERCENT SULFUR (MAX)
PULLMAN KELLOGG
LIMESTONE SCRUBBING
STARTUP   «*/80
                                      THIS NEW UNIT WILL BURN LOW SULFUR WESTERN COAL. 80 PERCENT OF THE
                                      GAS WILL BE SCRUBBED TO MEET SULFUR DIOXIDE EMISSION REGULATIONS.
                                      THE UTILITY ANNOUNCED THAT A CONTRACT HAS BEEN AWARDED TO PULLMAN/KELLOGG
                                      FOR THE INSTALLATION OF TWO WEIR HORIZONTAL CROSSFLOW SCRUBBING MODULES*
                                      THE CONTRACT FOR THE ELECTROSTATIC PRECIPITATOR HAS BEEN AWARDED
                                      TO JOY/WESTLRN PRECIPITATION DIVISION.  THE SULFUR DIOXIDE SCRUBBING
                                      REAGENT is LIMESTONE.  THE CONSULTING ENGINEERING AND CONSTRUCTION
                                      FIRM IS BECHTEL.
I.D. NUMBER   103
SALT RIVER PROJECT
CORONADO MO. 3
  350  HW - NEW
COAL 1.0 PERCENT SULFUR(MAY)
NOT SELECTED
LIMESTONE SCRUBBING
STARTUP   0/67
                                      THIS NEW UNIT WILL BURN LOW SULFUR WESTERN COAL. 80 PERCENT OF THE
                                      GAS WILL BE SCRUBBED TO MEET SULFUR DIOXIDE EMISSION REGULATIONS.
                                      THE UTILITY IS CURRENTLY CONSIDERING THE INSTALLATION OF TWO HORIZONTAL
                                      CROSSFLOW SCRUBBING MODULES EMPLOYING A LIMESTONE SCRUBBING SOLUTION
                                      TO REMOVE S02 FROM THE FLUE GAS.  SCHEDULED COMMERCIAL OPERATION
                                      DATE IS 1987.  PLANS FOR AN EMISSION CONTROL SYSTEM HAVE NOT
                                      BEEN FINALIZED.
 I.D. NUMBER   10«t
 SOUTH  CAROLINA  PUBLIC  SERVICE
 WINYAH NO. 2
   280   MW > NEW
 COAL   1.0 PERCENT  SULFUR
 BABCOCK & WILCOX
 LIMESTONE SCRUBBING
 STARTUP  5/77
                                      THIS NEW COAL-FIRED POWER BOILER WILL FIRE 1.0 PERCENT SULFUR COAL.
                                      PRIMARY PARTICULATE CONTROL WILL BE PROVIDED BY A HIGH-EFFICIENCY ESP
                                      (99.4 PERCENT). 50 PERCENT OF THE FLUE GAS FROM THIS 280-MW NOMINALLY
                                      RATED UNIT WILL BE SCRUBBED TO MEET NSPS. THE CONTRACT FOR THIS WET
                                      LIMESTONE SCRUBBING SYSTEM HAS BEEN AWARDED TO BABCOCK AND WILLCOX. THE
                                      GUARANTEED SULFUR DIOXIDE REMOVAL EFFICIENCY IS 69 PERCENT. SCRUBBING
                                      WASTES WILL BE DISPOSED IN AN ON-SlTE UNLINED SLUDGE POND.  THE UNIT
                                      IS NOW UNDER CONSTRUCTION.
 I.D. NUMBER   105
 SOUTHERN  CALIFORNIA  EDISON
 MOHAVE NO IB
  620  MW - RETROFIT
 COAL   0.5- 0.6 PERCENT  SULFUR
 NOT SELECTED
 LIME/LIMESTONE SCRUBBING
 STARTUP   6/77
                                      THE TOTAL CAPACITY OF BOILER IS 790 MW. EXISTING EXPERIMENTAL FGD MODULE
                                      WILL TREAT ONLY 170 MW.  FINAL SELECTION OF THE PROCESS HAS BEEN POST-
                                      PONED. SEE MOHAVL 1A.
                                                                31
                                                                                                  PEDCO ENVIRONMENTAL

-------
 COMPANY

 POWER STATION
           TABLE 2
STATUS OF FGO SYSTEMS DURING  12/76

                       CURRENT MONTH
1.0. NUMBER  106
SOUTHERN CALIFORNIA EDISON
MOHAVE NO. 2
  790  MW - RETROFIT
COAL   0.5 TO 0.8 % SULFUR
NOT SELECTED
LIME/LIMESTONE SCRUBBING
STAKTUP   6/77
    A PROTOTYPE 170 MW LIME SCRUBBING SYSTEM (HORIZONTAL MODULE) ON THIS UNIT
    WAS OPERATED FROM NOVEMBER 1973 UNTIL FEBRUARY 1975* AVAILABILITY FOR THE
    PERIOD l/16/7«* TO 2/9/75 AVERAGED 73.5S.  THIS SYSTEM IS TO BE REINSTALL-
    ED AT THE FOUR CORNERS PLANT* OPERATED BY ARIZONA PUBLIC SERVICE.
I.D. NUMBER  107
SOUTHERN ILLINOIS POWER COOP
SOUTHERN ILLINOIS POWER PT. «
  18f  MW - NEW
COAL
BABCOCK i WILCOX
LIMESTONE SCRUBBING
STARTUP   1/78
    THE CONTRACT FOR THIS LIMESTONE SCRUBBING SYSTEM HAS BEEN AWARDED TO
    BABCOCK AND WILCOX. THE FGD SYSTEM WILL CONSIST OF 2 SCRUBBING MODULES,
    TREATING THE FLUE GAS FROM A COAL-FIRED BOILER. HAVING A NOMINAL DESIGN
    CAPACITY OF 691»500 ACFM AT 290F. THE DESIGN S02 REMOVAL EFFICIENCY IS
    89.4 PERCENT, BASED UPON AN INLET OF 3,326 PPM OF S02. THE CONSULTING
    ENGINEERING FIKM FOR THIS PROJECT IS BURNS & MCDONNELL.
1.0. NUMBER  108
SOUTHERN INDIANA GAS4ELECTRIC
A.B. BROWN NO.l
  250  MM - NEW
COAL 3.75 PERCENT SULFUR
FMC CORPORATION
DOUBLE ALKALI SCRUBBING
STAKTUP   <*/79
    THIS NEW COAL-FIRED POWER-GENERATING UNIT IS PART OF A NEW POWER
    GENERATING STATION LOCATED IN WEST FRANKLIN,INDIANA.  THE UNIT
    WILL FIRE HIGH SULFUR(3.75 PERCENT) INDIANA COAL AND MUST
    COMPLY WITH NSPS.  THE UNIT'S EMISSION CONTROL SYSTEM WILL CONSIST
    OF AN ESP FOR PARTICULATE REMOVAL AND AN FGD SYSTEM FOR SULFUR
    DIUXIDE REMOVAL.  THE UTILITY HAS AWARDED A CONTRACT To THE FMC
    CORPORATION FOR THE INSTALLATION OF A DOUBLE ALKALI SCRUBBING
    SYSTEM UTILIZING SODA ASH AND LIME,  START-UP IS SCHEDULED FOR 0«»/79t
I.D. NUMBER  109
SOUTHERN MISSISSIPPI ELECTRIC
R.D. MORROW NO.l
  180  MW - NEW
COAL 1.0 PERCENT SULFUR
RILEY STOKER / ENVlRONEERING
LIMESTONE SCRUBBING
STARTUP  11/77
    THIS NEW COAL-FIRED UNIT WILL FIRE 1.0 PERCENT SULFUR COAL. A CONTRACT
    HAS BEEN AWARDED TO RILEY STOKER/ENVIRONEERING FOR THE INSTALLATION OF
    A WET LIMESTONE SCRUBBING SYSTEM. PARTICULATES WILL BE CONTROLLED BY A
    HIGH-EFFICIENCY ESP UPSTREAM OF THE SCRUBBING SYSTEM. DESIGN SULFUR
    DIOXIDE AND PARTICULATE REMOVAL EFFICIENCIES ARE 85 AND 99.6 PERCENT,
    RESPECTIVELY. SCRUBBER SLUDGE WILL BE STABILIZED WITH FLYASH AND DISPOSED
    ON THE PLANT SITL.  CONSTRUCTION OF THE SCRUBBING SYSTEM IS NOW IN
    PROGRESS.  ERECTION OF THE ABSORBER TOWERS HAS BEEN COMPLETED.
I.D. NUMBER  110
SOUTHERN MISSISSIPPI ELECTRIC
R.D. MORROW NO.2
  ISO  MW - NEW
COAL 1.0 PERCENT SULFUR
RILEY STOKER / ENVlRONEERING
LIMESTONE SCRUBBING
STARTUP   6/78
     THIS NEW  COAL-FIRED  UNIT  WILL FIRE  1.0 PERCENT SULFUK COAL. A CONTRACT
     HAS UEEN  AWARDED  TO  RILEY STOKER/ENVIRONEERING FOR  THE  INSTALLATION OF
     A  WET LIMESTONE SCRUBBING SYSTEM. PARTICULATES WILL BE  CONTROLLED  BY  A
     HIGH-EFFICIENCY ESP  UPSTREAM OF  THE SCRUBBING SYSTEM. DESIGN SULFUR
     DIOXIDE AMD PARTICULATE REMOVAL  EFFICIENCIES ARE  85 AND 99.6 PERCENTt
     RESPECTIVELY.  SCRUBBER SLUDGE WILL  BE STABILIZED  WITH FLYASH AND DISPOSED
     ON THE PLANT SITE. ERECTION OF THE  ABSORBER TOWERS  IS NOW  IN PROGRESS.
                                                                32
                                                                PEDCO ENVIRONMENTAL

-------
 COMPANY
           TABLE 2
STATUS OF FGO SYSTEMS DURING  12/76
 POWER STATION
                       CURRENT MONTH
1.0. NUMBER  111
SPRINGFIELD CITY UTILITIES
SOUTHWEST NO. 1
  200  MW -NEW
COAL 3.5 PERCENT SULFUR
UNIVERSAL OIL PRODUCTS
LIMESTONE SCRUBBING
STARTUP   2/77
    THE BOILER AND ELECTROSTATIC PREClPITATOR ARE NOW OPERATIONAL* THE
    SCRUBBERS ARE BEING BYPASSED UNTIL CONSTRUCTION is COMPLETED. THE
    MAJORITY OF THE CONSTRUCTION ON THE SCRUBBING SYSTEM HAS BEEN COMPLETED.
    INITIAL OPERATION OF THE SCRUBBING SYSTEM WILL COMMENCE ON FEB It 1976.
    COMMERCIAL OPERATION WILL FOLLOW 60 DAYS LATER. INSTALLATION OF THE
    SYSTEM HAS BEEN HAMPERED BY SOME WIRING PROBLEMS IN THE SCRUBBING AND
    SLUDGE TREATMENT EQUIPMENT. PARTICULATES WILL BE CONTROLLED BY A HIGH-
    EFFICIENCY ESP INSTALLED UPSTREAM OF THE SCRUBbER MODULES.
1.0. NUMBER  112
TENNESSEE VALLEY AUTHORITY
SHAWNEE N0.10A
   10  MU - RETROFIT
COAL 2.9 PERCENT SULFUR
UNIVERSAL OIL PRODUCTS
LIME/LIMESTONE  SCRUBBING
STARTUP   
-------
 COMPANY

 POWER STATION
           TABLE 2
STATUS OF F60 SYSTEMS OUR INS  12/7(6

                       CURRENT MONTH
1.0. NUMBER  116
TEXAS UTILITIES CO.
MARTIN LAKE NO. 2
  793  MW - NEW
COAL   1*0 PERCENT SULFUR
RESEARCH COTTRELL
LIMESTONE SCRUBBING
STARTUP  10/77
    THE CONTRACT FOR THIS F6D SYSTEM WAS AWARDED TO RESEARCH-COTTRELL. THIS
    NEW FACILITY IS NOW UNDER CONSTRUCTION. THE FGD SYSTEM STARTUP DATE IS
    NOW SCHEDULED FOR OCTOBER 1977.
1.0. NUMBER  117
TEXAS UTILITIES CO.
MARTIN LAKE NO. 3
  793  MW - NEW
COAL 1.0 PERCENT SULFUR
RESEARCH COTTRELL
LIMESTONE SCRUBBING
STARTUP  12/76
    THE CONTRACT FOR THIS FGD SYSTEM HAS BEEN AWARDED TO RESEARCH-COTTRELL.
    THE BOILER IS NOW BEING ERECTED. START-UP IS SCHEDULED FOR DECEMBER
    1978.
I.D. NUMBER  118
TEXAS UTILITIES CO.
MARTIN LAKE NO. t
  793  MW - NEW
COAL 1.0 PERCENT SULFUR
RESEARCH COTTRELL
LIMESTONE SCRUBBING
STARTUP  12/79
    THE CONTRACT FOR THIS FGD SYSTEM HAS BEEN AWARDED TO RESEARCH-COTTRELL.
    THE BOILER IS NOW BEING ERECTED. START-UP IS SCHEDULED FOR DECEMBER
    1978.
I.D. NUMBER  119
TEXAS UTILITIES CO.
MONTICELLO NO.3
  750  HW - NLW
LIGNITE 1.0 PERCENT SULFUR
CHEMICO
LIMESTONE SCRUBBING
STARTUP  10/77
    THIS NEW STEAM BOILER WILL FIRE LOW SULFUR (0.8 TO 1.0 PERCENT SULFUR)
    TEXAS LIGNITE. THE EMISSION CONTROL SYSTEM FOR THIS UNIT CONSISTS OF
    A HIGH EFFICIENCY ESP UPSTREAM OF LIMESTONE SPRAY TOWERS. THE CONTRACT
    FOR THIS SCRUBBING SYSTEM HAS BEEN AWARDED TO CHEMICO FOR THE INSTAL-
    LATION OF THE SPHAY TOwERS. THE ESP IS A COLD-SIDE UNIT SUPPLIED BY POL-
    LUTION CONTKOL-WALTHER. DESIGN PARTICULATE AND SULFUK DIOXIDE REMOVAL
    EFFICIENCY WILL ENABLE THIS UNIT TO MEET NEW SOURCE PERFORMANCE STANDARDS
I.D. NUMBER  120
UNITED POWER ASSOCIATION
COAL CREEK NO. 1
  5
-------
 COMPANV

 POWER STATION
           TABLE 2
STATUS OF FGO SYSTEMS DURING  12/76

                       CURRENT MONTH
1.0. NUMBER  121
UNITED POWER ASSOCIATION
COAL CREEK NO. 2
  545  MW - NEW
LI6NITE - 0.63 PERCENT SULFUR
COMBUSTION ENGINEERING
LIKE SCRUBBING
STARTUP  11/79
    THE CONTRACT FOR THIS SCRUBBING SYSTEM HAS BEEN AWARDED TO COMBUSTION
    ENGINEERING FOR THE INSTALLATION OF LIME FGD SYSTEMS ON UNITS NOS.l AND
    2 AT THIS STATION. THE SCRUBBING SYSTEM FOR EACH BOILER WILL CONSIST OF
    4 SPAY TOWER ABSOBER MODULES FOK REMOVING S02 FROM THE FLUE GAS.
    ELECTROSTATIC PRECIPITATORS WILL BE INSTALLED UPSTREAM OF EACH SCRUBBING
    SYSTEM. FULL COMMERCIAL START-UP DATES FOR UNITS 1 AND 2 ARE 11/78 AND
    11/79 RESPECTIVELY. INITIAL OPERATIONS WILL COMMENCE THE PRECEDING
    AUGUST FOR E\CH UNIT.  F&D CONSTRUCTION IS SCHEDULED TO COMMENCE On/78.
1.0. NUMBER  122
UTAH POWER & LIGHT CO.
EMERY NO.l
  400  MM . NEW
COAL 0.5 PERCENT  SULFUR
CHEMICO
LIME: SCRUBBING
STARTUP   6/76
    A CONTRACT HAS BEEN AWARDED TO THE CHEMICO AIR POLLUTION DIVISION FOR
    A PEBBLE LIME WET SCRUBBING SYSTEM ON THIS NEW UNIT. THE SCRUBBING
    SYSTEM IS DESIGNED TO OPERATE IN AN OPEN WATER LOOP MODE WITH AN S02
    REMOVAL EFFICIENCY OF 60 PERCENT FOR LOW SULFUR UTAH COAL. PRIMARY
    PAKTICULATE CONTROL WILL BE PROVIDED BY AN ESP UPSTREAM OF THE SCRUBBERS.
    THE SCRUBBER SLUDGE WILL BE STABILIZED WITH FLYASH AND DISPOSED ON THE
    PLANT SITE.  THE A-E DESIGN FIRM FOR THIS PROJECT IS STEARNS-ROGER.
 I.D.  NUMBER  123
 UTAH  POWER & LIGHT CO.
 HUNTINGTON NO.l
   <415  MW - NEW
 COAL   0.5 PERCENT SULFUR
 CHEMICO
 LIME  SCRUBBING
 STARTUP   6/77
    A CONTRACT HAS BEEN AWARDED TO CHEMICO AIR POLLUTION DIVISION FOR
    A LIME SCRUBBING SYSTEM ON THIS NEW UNIT. MATERIALS ARE NOW ARRIVING AT
    THE PLANT SITE. SITE PREPARATION AND CONSTRUCTION IS NOW UNDERWAY. THE
    STATE OF UTAH REGULATIONS REQUIRE THE BEST AVAILABLE AND MOST COST
    EFFECTIVE TECHNOLOGY FOR SULFUR DIOXIDE REMOVAL. PRIMARY PARTICULATE
    REMOVAL WILL BE PROVIDED BY AN ESP INSTALLED UPSTREAM OF THE WET
    SCRUBBING SYSTEM. THE A-E DESIGN FIRM FOR THIS PROJECT IS STEARNS-ROGER.
 I.D.  NUMBER  124
 WISCONSIN POWER & LIGHT CO.
 COLUMBIA NO. 2
   527  MW - NEW
 COAL  0.8 PERCENT SULFUR
 NOT SELECTED
 LIME/LIMESTONE SCRUBBING
 STARTUP   1/80
     THE UTILITY  IS NOW REQUESTING/EVALUATING BIDS FOR A NEW COAL-FIRED UNIT
     CURRENTLY UNDER CONSTRUCTION AT THEIR COLUMBIA STATION LOCATED IN PORTAGE
     WISCONSIN. START-UP OF THE BOILER IS SCHEDULED FOR MARCH 1978. START-UP
     OF THE SCRUBBING SYSTEM IS PROJECTED FOR JANUARY 1980. THE UNIT WILL
     COMPLY WITH  STANDARDS DURING THE INTERIM BY BURNING LOW SULFUR BELAIR
     COAL. THE SCRUBBERS ARE BEING DESIGNED TO TREAT 50 PERCENT OF THE FLUE
     GAS RESULTING FROM THE COMBUSTION OF LOW SULFUR COLSTRlP COAL. THE RE-
     MAINING 50 PERCENT WILL BE BYPASSED FOR REHEAT.
                                                                 35
                                                                PEDCO ENVIRONMENTAL

-------

-------
                     TABLE  3




PERFORMANCE DESCRIPTION FOR OPERATIONAL FGD SYSTEMS
                           37                PEDCO-ENVIRONMENTAL

-------
PCOCO

-------
                  TABLE 3
PERFORMANCE DESCRIPTION FOR OPERATIONAL F6D SYSTEMS  12/76
 IDENTIFICATION NO.

 UTILITY NAME

 UNIT NAME

 UNIT LOCATION

 UNIT RATING
ARIZONA PUBLIC SERVICE

CHOLLA NO 1

JOSEPH CITY  ARIZONA

  115  MU
 FUEL CHARACTERISTICS  COAL   0.
-------
                                                           BACKGROUND INFORMATION
                                                                     ON
                                                           THE CHOLLA POWER PLANT
     THE CHOLLA POWER STATION*  LOCATED NEAR JOSEPH CITY,  ARIZONA,  HAS ONE 115-MW COAL-FIRED BOILER IN SERVICE AND TWO 250  MW UNITS
UNDER CONSTRUCTION.  CHOLLA NO. 1 IS A DRY-BOTTOM PULVERIZED-COAL-FIRED UNIT DESIGNED BY COMBUSTION ENGINEERING.   THE AVERAGE
CHARACTERISTICS OF THE COAL BURNED DURING THE COURSE OF 1975 ARE*   HEAT CONTENT OF 10*150 BTU/LB* ASH CONTENT OF  13.US PERCENT*
SULFUR CONTENT OF 0.52 PERCENT* CHLORIDE OF 0.04 PERCENT  (MAX.)* AND MOISTURE CONTENT OF 14.77 PERCENT.
     THE FGD SYSTEM AT THE CHOLLA PLANT WAS MANUFACTURED  BY RESEARCH-COTTRELL AND INSTALLATION WAS COMPLETED ON DECEMBER 3,  1973.
THE DESIGN COMBINED SULFUR UIOXIDE REMOVAL EFFICIENCY (FOR BOTH MODULES A AND B) IS 58.5 PERCENT.  THE SYSTEM CONSISTS OF  TWO
PARALLEL TRAINS (MODULES A AND  B).  EACH TRAIN IS DESIGNED FOR 240,000 ACFM THROUGHPUT AT 276 F,  AND HANDLES APPROXIMATELY 50
PERCENT OF THE BOILER'S FLUE GAS LOAD.  THE A SIDE CONSISTS OF A VARIABLE THROAT FLOODED DISC SCRUBBER FOS FOLLOWED BY A PACKED
TOWER (HUNTERS PACKING).  THE B-SIDE IS SIMILAR IN DESIGN.  HOWEVER, THE TOWER IS NOT PACKED AND  LIMESTONE SLURRY IS NOT CIRCU-
LATED THROUGH IT.  EITHER ONE OR BOTH OF THE SCRUBBERS CAN BE BYPASSED.  GAS LEAKAGE AROUND EACH  TRAIN IS ESTIMATED TO BE  ABOUT
4.5 PERCENT OF THE GAS BEING TREATED.  THE TOWER PACKING, WHICH IS APPROXIMATELY 2-FEET THICK, IS CONSTRUCTED OF  POLYPROPYLENE
CORRUGATED SHEETS JOINED TOGETHER IN CRISS-CROSS PATTERNS SIMILAR  TO HONEYCOMBS.  THE TOWER DEMISTERS ARE ALSO CONSTRUCTED OF
POLYPROPYLENE, AND THE REHEATERS ARE SHELL AND TUBE TYPE  CONSISTING OF THREE TUBE BUNDLES PER UNIT.
     LIMESTONE FOR THE FGO SYSTEM IS PURCHASED IN GROUND FORM SUITABLE FOR SLURRYING.  THE MAIN SOURCE OF SUPPLY  IS THE SUPERIOR
CO.  LOCATED NEAR PHOENIX, ARIZONA.  THIS GRADE OF LIMESTONE IS GENERALLY KNOWN AS *RED WALL* LIMESTONE AND IS CONSIDERED  A VERY
HIGH QUALITY GRADE.  CHEMICAL SPECIFICATIONS ARE*  MINIMUM CALCIUM OXIDE CONTENT, 52 PERCENT* MINIMUM CALCIUM CARBONATE CONTENT,
95 PERCENT* MAXIMUM MAGNESIUM OXIDE CONTENT, 2 PERCENT* MAXIMUM MAGNESIUM CARBONATE CONTENT, 0.5 PERCENT* MAXIMUM SILICA CONTENT,
1 PERCENT.
     THE PLANT HAS NO SLUDGE TREATMENT OR FIXATION SYSTEMS.  THE SLUDGE IS PUMPED TO THE FLY ASH POND ON AN INTERMITTENT BASIS
THROUGH A COMMON PIPING SYSTEM WITH THE FLY ASH.  NO POND WATER IS RECYCLED TO THE FGO SYSTEM (SOLAR EVAPORATION  POND), A GENERAL
PROCESS FLOW DIAGRAM OF THE CHOLLA FGO SYSTEM IS PRESENTED IN FIGURE 1, APPENDIX C.

-------
CHOLLA POWER PLANT (CONTINUED)
PROBLEMS AND SOLUTIONS
     DECEMBERt 1973 TO APRIL 2, 197H - BECAUSE OF A DIFFERENCE IN SIZE OF THE MAIN DUCT AND THE REHEATER TRANSITION DUCT* THE GAS
FLOW PRODUCED HARMONIC VIBRATIONS IN THE REHEATER.  THE VIBRATIONS WERE PARTIALLY DAMPED BY INSTALLATION OF BAFFLES.  ONE OF THE
REHEATER TUBE BUNDLES WAS BADLY CORRODED BY ACID THAT CONDENSED IN THE UNINSULATED DUCT UPSTREAM OF THE REHEATERS.  THE TUBE
BUNDLE WAS REPLACED* AND A BAFFLE WAS INSTALLED TO DIVERT CONDENSED ACID FROM REHEATER TUBES.  ALSO* THE DUCT UPSTREAM OF THE
REHEATER MAS INSULATED.  THE ACID CONDENSATION OCCURRED ONLY IN THE MODULE WITH NO TOWER PACKING AND HENCE LOW SULFUR DIOXIDE
REMOVAL EFFICIENCY.
     ANOTHER PROBLEM RESULTED  BECAUSE OF SOLIDS BUILDUP IN THE FOS STUFFING GLAND BOX AND ON TOP OF THE SPRAY DOME.  ALSO, SOME
LINES PLUGGED* PARTICULARLY WHEN THE SYSTEM OPERATED  AT LOW FLOW RATES.  SOLIDS SETTLED OUT IN STANDBY PUMPS, AND EXCESSIVE FAN
VIBRATIONS  OCCURRED  BECAUSE OF ACCUMULATION OF SCALE  BUILDUP WHEN THE UNIT WAS IDLE.  TO SOLVE THESE PROBLEMS, PACKING GLAND
POSITION  WAS  REVERSED  (INSTALLED UPSIDE DOWN), THE FAN WAS SANDBLASTED,  THE PIPING WAS MODIFIED TO  ELIMINATE STAGNANT POCKETS, AND
PUMPS WERE  FLUSHED IMMEDIATELY AFTER  REMOVAL  FROM SERVICE.
      OPERATION OF THE  SYSTEM  THROUGHOUT 1975  AND  1976 RESULTED  IN THE DEVELOPMENT OF SOME ADDITIONAL PROBLEM AREAS, INCLUDING*
SIGNIFICANT CORROSION  ATTACK  IN THE VESSEL WAULS  OF THE j-LOOOED-OISC PARTICULATE SCRUBBER MODULE* ACID CORROSION  IN THE B-SIDE
REHEATER  HOUSING* SCALE BUILDUP IN THE  PIPE OUTLET AT THE SLUDGE/FLY ASH EVAPORATION POND* PLUGGING IN THE SCRUBBER TOWER PACKING
 AND MIST  ELIMINATOR* EROSION  IN THE PUMPS* CORROSION  IN THE BOILER EXHAUST ELBOW OF THE DUCTWORK LEADING FROM THE SCRUBBERS TO THE
 STACK.
                                                                »1                                PEDCO ENVIRONMENTAL

-------
                                                           FGO SYSTEM RELIABILITY

                                                              CHOLLA UNIT NO.  1

                    RELIABILITY (X)
MONTH          MODULE A       MODULES                                          COMMENTS

JAN. 74           97             90

FEB. 74          100             94

MAR. 74          100             66

APR. 74           66             57

MAY  74           96             99

JUN. 74          100            100

JUL. 74           97             92

AU6. 74           97             97

SEP. 74           95             99

OCT. 74           63             66           ANNUAL BOILER AND FGD SYSTEM OVERHAUL.

NOV. 74          100             96

DEC. 74          100            100

JAN. 75           98             99

FEB. 75           96             99

MAR. 75

APR. 75           88             65

MAY  75           46             40           MODULES WERE BOTH OFF-LINE FOR MOST OF MONTH FOR SCHEDULED REPAIRS AND CLEANING.

JUN. 75          100            100           SUBSTANTIAL PLUGGING OF PACKING AND MIST ELIMINATORS WAS OBSERVED.

                                                                                                              NO PROBLEM REPORTED.

JUL. 75           97             98           MODULES WERE SHUT DOWN TO CLEAN FLOW RESTRICTIONS IN FLOODED-DISC RECIRCULATION

                                             LINES.

AUG. 75           95            100           MODULE A WAS DOWN FOR INSPECTION ONE TIME.

-------
                                                           FGO SYSTEM RELIABILITY
                                                        CHOLLA UNIT NO. 1 (CONTINUED)
                    RELIABILITY (X)
MONTH          MODULE A       MODULE B                                          COMMENTS
SEP. 75           98             97          MINOR OUTAGE DUE TO FLOOOEO-OISC LINES.
OCT. 75           6
-------
                                                           F6D SYSTEM RELIABILITY

                                                        CHOLLA UNIT NO.  1 I CONTINUED)

                    RELIABILITY <»>
MONTH          NODULE A       MODULE B                                          COMMENTS

JUL. 76          100             98           DURING THE JULY-AUGUST PERIOD THE UTILITY REPORTED THAT REPAIRS TO THE COATIN6 IN THE

AUG. 76          100            100           ELBOW OF THE SCRUBBER EXHAUST DUCT WERE COMPLETED.  A MALFUNCTIONING SELENOID VALVE

                                             IN THE DEMISTER WASH SYSTEM OF THE B-SIDE TRAIN PREVENTING INADEQUATE WASHING OF

                                             THE DEMISTER, RESULTED IN A MINOR SCRUBBER OUTAGE.  THE BOILER WAS IN SERVICE THE

SEP. 76          100            100           THE ENTIRE MONTH.  THE A-SIOE WAS IN SERVICE 720 HR.t THE B-SIDE 676 HOURS.   NO

                                             SIGNIFICANT PROBLEMS WERE REPORTED.

OCT. 76           56             56           THE BOILER WAS IN SERVICE 417 HOURS DURING THE MONTH.  A-SlOE AND B-SIDE OPERATIONAL

                                             HOURS WERE 415 AND 277 RESPECTIVELY.

NOV. 76           96             98           DURING THE MONTH THE BOILER A-SIDE AND B-SIDE TRAINS WERE IN SERVICE 720t 682 AND 556

                                             HOURS, RESPECTIVELY. TWO MINOR FORCED SCRUBBER OUTAGES OCCURRED DURING THE PERIOD

                                             BECAUSE A REHEATER STEAM LEAK AND INLET GAS DAMPER ADJUSTMENTS TO BOTH THE A-SIOE AND

                                             B-SIDE SCRUBBING TRAINS.

DEC. 76           96            100           BOILER, A-SIDE, AND B-SIDE OPERATION HOURS FOR THE MONTH WERE 714, 742 AND 498 HOURS,

                                             RESPECTIVELY. ONE OUTAGE WAS REPORTED BECAUSE OF AN ADDITIONAL ADJUSTMENT TO THE

                                             A-SIDE GAS INLET DAMPER.
                                                                                                  PCDCO ENVIRONMENTAl.

-------
                  TABLE 3
PERFORMANCE DESCRIPTION FOR OPERATIONAL F60 SYSTEMS  12/76
 IDENTIFICATION NO.

 UTILITY NAME

 UNIT NAME

 UNIT LOCATION

 UNIT RATING

 FUEL CHARACTEKISTICS

 FGD VENDOR

 PROCESS

 NEW OR RETROFIT

 START  UP DATE

 FGD STATUS

 EFFICIENCY,
   PARTICULATES


   S02


  WATER MAKE  UP


  SLUDGE DISPOSAL


  UNIT COST
 10

ARIZONA PUBLIC SERVICE

FOUR CORNERS NO. 5A

FARMINGTON NEW MEXICO

 160 MW

COAL  0.7 PERCENT SULFUR

SO. CALIFORNIA EDISON

LIME SCRUBBING

RETROFIT

 2/76

OPERATIONAL
  OPERATIONAL
   EXPERIENCE
 REFER TO THE BACKGROUND INFORMATION SECTION IN TABLE  3 OF THIS REPORT.
 PENDING THE OUTCOME OF  TESTS  WHICH HAVE JUST BEEN COMPLETED ON THE
 MOVED FROM THE MOHAVE TEST  SITE AND REASSEMBLED AT THE FOUR CORNERS
 STATION OF ARIZONA PUBLIC SERVICE. THE EXPERIMENTAL MODULE IS DESIGNED
 TO TREAT APPROXIMATELY  20 PERCENT OF THE FLUE GAS FLOW FROM UNIT NO. 5
 WHICH HAS A NET GENERATING  CAPACITY, OF 75S-MW. THE S02 TEST PROGRAM
 COMMENCED FEB. 1976 AND WAS COMPLETED ON DEC. 6, 1976. UPON CONCLUSION OF
 THE PROGRAM, THE MODULE WAS DISASSEMBLED. RESULTS WILL BE PUBLISHED
                                                                                               PEOCO ENVIRONMENTAL

-------
                                                           BACKGROUND  INFORMATION



                                                                 ON



                                           FOUR  CORNERS  NO. 5A -  EXPERIMENTAL  HORIZONTAL  SCRUBBER



     THE FOUR CORNERS POWER STATION,  LOCATED NEAR  FARMINGTON,  NEW MEXICO,  IS JOINTLY  OWNED  BY  THE  ARIZONA PUBLIC  SERVICE COMPANY



AND THE SOUTHERN CALIFORNIA EDISON COMPANY.  THIS  STATION CONTAINS FIVE  COAL-FIRED  BOILERS  WITH AN EQUIVALENT  ELECTRIC  POWER



GENERATING CAPACITY OF 2233-MW.   ONLY UNIT NO. 5 IS  RETROFITTED WITH AN  FGD SYSTEM.



     UNIT NO. 5 IS A COAL-FIRED  BOILER CAPABLE OF  GENERATING 5»«»H6»000 LBS. OF STEAM,  WHICH IS EQUIVALENT TO 800-MW  OF  NET  ELEC-



TRICAL POWER.  THIS UNIT WAS FIRST PLACED IN COMMERCIAL  OPERATION JULY 1970. APPROXIMATELY  20  PERCENT  OF THE FLUE GAS GENERATED BY



THIS BOILER IS BEING SCRUBBED INITIALLY IN ORDER TO  ESTABLISH WHAT SULFUR  DIOXIDE AND PARTICULATE  REMOVAL EFFICIENCIES  CAN  BE



OBTAINED.



     THE FGO SYSTEM WHICH HAS BEEN RETROFITTED ON  UNIT NO. s is THE WEIR HORIZONTAL CROSSFLOW  SPRAY SCRUBBER WHICH WAS  FORMERLY



INSTALLED AND OPERATED IN A TEST PROGRAM AT THE  MOHAVE GENERATING STATION  OF THE SOUTHERN CALIFORNIA EDISON COMPANY(SEE MOHAVE NO.



2A IN APPENDIX A OF THIS REPORT).



     DURING THE MOHAVE TEST PROGRAM THE HORIZONTAL MODULE WAS OPERATIONAL  FROM NOVEMBER 1«  1973, TO JANUARY 16,1974, FOR SHAKEDOWN



PURPOSES.  OVER THE COURSE OF THE ACTUAL TEST PROGRAM* WHICH EXTENDED  FROM JANUARY  16, 197H, TO FEBRUARY 9, 1975* THE PROTOTYPE



UNIT OPERATED A TOTAL OF 5,927 HOURS IN VARIOUS  TEST MODES.  FOLLOWING COMPLETION OF  TESTS, THE MODULE WAS SHUT DOWN, DISMANTLED*



TRANSPORTED, AND REASSEMBLED AT  THE FOUR CORNERS GENERATING STATION OF ARIZONA PUBLIC SERVICE  FOR  FURTHER TESTING.



     THE HORIZONTAL MODULE IS A FOUR-STAGE SCRUBBING CHAMBER WITH THE  FOLLOWING DIMENSIONS* LENGTH -  US FEET* WIDTH -  26 FEET*



HEIGHT - 15 FEET.  THE MODULE ITSELF IS A HOLLOW CHAMBER CONSISTING OF FOUR STAGES  OF CROSSFLOW SPRAY  NOZZLES. EACH  STAGE CONTAINS



A ROW OF 36 EXTERNALLY-MOUNTED NOZZLES.  THE SLURRY  IS CYCLED THROUGH  THE  SCRUBBER  IN A COUNjERCURRENT MANNER  AT A RATE OF  36,000



GPM/STAGE.  FRESH LIME SLURRY IS SPRAYED ACROSS THE  FLUE GAS AT THE  FOURTH STAGE,  WHICH  IS  THE DISCHARGE END OF THE  SCRUBBING



CHAMBER.  THE SCRUBBING SOLUTION IS THEN COLLECTED AND RECYCLED SUCCESSIVELY  TO THE THIRD,SECOND,AND FIRST STAGES OF THE SCRUBBING



MODULE.  THIS ALLOWS FOR COMPLETE DEPLETION OF  ANY EXCESS ALKALINITY  AND INSURES THAT FRESH SLURRY IS  CONTACTING GAS HAVING THE



LOWEST SUFLUR DIOXIDE CONCENTRATION.  THE LI8UID RECIRCULATION RATE  CAN  BE ADJUSTED OVER  A  WIDE RANGE.  THE MODULE IS  DESIGNED TO



TREAT A MAXIMUM FLUE GAS CAPACITY OF 
-------
FOUR CORNERS NO. 5A (CONTINUEED)



SCRUBBING SYSTEM TO A THICKENER AND THE UNDERFLOW IS PUMPED TO AN ON-SITE SETTLING POND.  WATER IS RETURNED TO THE PROCESS FOR




FURTHER USE.



     A CUTAWAY VIEW OF THE WEIR SCRUBBING CHAMBER IS PRESENTED IN FIGURE 2 OF APPENDIX C.
                                                                                                  PEOCO ENVIRONMENTAL

-------
                                                   FOUR  CORNERS NO.  5A
PERIOD
MONTH/YEAR

FEB. 76

MAR. 76
APR. 76

HAY  76

JUN. 75

JUL. 76

AUG. 76

SEP. 76

OCT. 76

NOV. 76

DEC, 76
     OPERATING HOURS
BOILER         F60 SYSTEM
COMMENTS
                                    INSTALLATION OF THE MODULE AT THE FOUR CORNERS GENERATING STATION WAS

                                    COMPLETED AND THE MODULE WAS PLACED IN-SERVICE FEBRUARY 17. 1976.

                                    FOR INITIAL OPERATION.

                                    THE SYSTEM WAS TAKEN DOWN IN MID-APRIL FOR A SCHEDULED BOILER OVERHAUL,

                                    SYSTEM RESTART IS SCHEDULED FOR JULY 1976.



                                    THE SYSTEM HAS REMAINED OUT OF SERVICE SINCE MID-APRIL 1976 BECAUSE OF AN

                                    EXTENSIVE OVERHAUL TO THE NO, 5 BOILER PLUS THE DEVELOPMENT OF PROBLEMS

                                    WITH THE SCRUBBER MODULE'S REHEATER UNIT.



                                    THE PROTOTYPE WAS IN SERVICE THROUGHOUT THE MONTH OF NOVEMBER. ON DEC.6 THE TEST

                                    PROGRAM WAS CONCLUDED AND THE UNIT HAS SINCE BEEN DISMANTLED.  APS IS NOW IN THE

                                    PROCESS OF ANALYZING THE OPERATING DATA ACCUMULATED DURING THE TEST PERIOD. A

                                    REPORT ADDRESSING THE RESULTS OF THE PROGRAM WILL BE PUBLISHED IN FEBRUARY 1977.
                                                                                                  PEOCO ENVIRONMENT M_

-------
                  TABLE 3
PERFORMANCE DESCRIPTION FOR OPERATIONAL F60 SYSTEMS  12/76
 IDENTIFICATION NO.
 UTILITY NAME
 UNIT NAME
 UNIT LOCATION
 UNIT RATING
  19

CENTRAL  ILLINOIS LI6HT CO.

DUCK CKEEK NO.  1A

CANTON ILLINOIS

  100 MW
 FUEL CHARACTERISTICS  COAL 2.5 - 3.0 PERCENT SULFUR
 FGD VENDOR

 PROCESS

 NEW OR RETROFIT

 START UP DATE

 F6D STATUS

 EFFICIENCY,
  PARTICULATES
 RILEY STOKER / ENVIRONEERING

 LIMESTONE SCRUBBING

 NEW

  9/76

 OPERATIONAL


 99.6 PERCENT
  S02
 75 PERCENT
 WATEK MAKE UP
 CLOSED LOOP
 SLUDGE DISPOSAL
 UNSTABILI2ED* SLUDGE DISPOSED IN LINED POND
 UNIT COST
$80/KW CAPITAL (ESTIMATED)
 OPERATIONAL
  EXPERIENCE
 THE INSTALLATION OF THIS SINGLE 100-MW SCRUBBER NODULE WAS COMPLETED IN
 JULY AND START-UP OPERATIONS FOLLOWED. DEBUGGING OPERATIONS HAVE BEEN
 PROCEEDING ON AN INTERMITTENT BASIS BECAUSE OF CONSTRUCTION-RELATED
 PROBLEMS. THE SYSTEM WAS SHUTDOWN FOR A SHORT  PERIOD OF TIME TO  CORRECT
 THESE PROBLEMS. RE-START COMMENCED ON SEPTEMBER 9.  OPERATION OF  THE
 MODULE DURING THE PERIOD FOLLOWING START-UP HAS BEEN INTERMITTENT BECAUSE
 OF MECHANICAL ANO CHEMICAL-RELATED PROBLEMS. THIS HAS PROMPTED THE
 UTILITY TO SHUTDOWN THE MODULE UNTIL FULL-SCALE START-UP DATE OF 6/7S.
                                                                                               PEOCO ENVIRONMENTAL

-------
                  TABLE 3
PERFORMANCE DESCRIPTION FOR OPERATIONAL F60 SYSTEMS  12/76
 IDENTIFICATION NO.

 UTILITY NAME

 UNIT NAME

 UNIT LOCATION

 UNIT RATING

 FUEL CHARACTERISTICS

 FGD VENDOR

 PROCESS

 NEW OR RETROFIT

 START UP DATE

 FGD STATUS

 EFFICIENCY,
  PARTICULATES
 31

 COMMONWEALTH EDISON

 WILL COUNTY NO 1

 ROMEOVILLE ILLINOIS

 167 HW

 COAL 4.0 PERCENT SULFUR

 BABCOCK & WILCOX

 LIMESTONE SCRUBBING

 RETROFIT

 2/72

 OPERATIONAL


 98 PERCENT
   S02
 62 PERCENT
  WATER  MAKE UP
 OPEN LOOP
  SLUU6E DISPOSAL
  STABILIZED SLUDGE DISPOSED IN  HAULAWAY TO LANUFILL
 UNIT COST
S113/KW CAPITAL * 13 HILLS PERKWH OPERATING
 OPERATIONAL
  EXPERIENCE
 REFER TO THE BACKGROUND INFORMATION SECTION IN TABLE 3 OF THIS REPORT.
 THIS FULL SCALE DEMONSTRATION SCRUBBING SYSTEM HAS BEEN IN SERVICE SINCE
 FEBRUARY 1972.  THE FGD SYSTEM INCLUDES TWO SCRUBBING TRAINS FOR THE
 CONTROL OF PARTICULATES AND SULFUR DIOXIDE. MODULE AVAILABILITY.
 OPERABILITY,  RELIABILITY,  AND UTILIZATION INDEX VALUES FOR THE PERIOD
 ARE  POSTED IN TABLE THRLE.  THE BOILER FIRED BOTH LOW SULFUR
 WESTERN COAL  AND HIGH  SULFUR ILLINOIS COAL DURING SEPARATE MONTHS.
 THE  FIXATION  AHO HAULAWAY  OF SCRUBBER WASTES CONTINUED DURING THE PERIOD.
                                                                                               PEOCO ENVIRONMENTAL

-------
                                                     BACKGROUND INFORMATION



                                                              ON



                                                       WILL COUNTY NO. 1



     IN 1970t COMMONWEALTH EDISON CONTRACTED WITH THE BECHTEL CORPORATION TO INVESTIGATE THE SULFUR REMOVAL SYSTEMS THEN AVAILABLE



HAVING A SUFFICIENT DEGREE OF DEVELOPMENT TO WARRANT LARGE-SCALE INSTALLATION ON WILL COUNTY STATION'S UNIT NO. I.  AFTER DECIDING



ON A WET SCRUBBER SYSTEM USING LIME OR LIMESTONE* BECHTEL PREPARED A SPECIFICATION AND RELEASED IT FOR BID. FROM NINE BIDDERS THAT



WERE SOLICITED, SEVEN PROPOSALS WERE RECEIVED.  AFTER DETAILED STUDY AND BIO EVALUATION WITH SPECIAL CONSIDERATION OF THE PROJECT



SCHEDULE, BABCOCK AND WILCOX WAS AUTHORIZED IN SEPTEMBER 1970 TO BEGIN DETAILED ENGINEERING FOR A LIMESTONE SLURRY SYSTEM.  COM-



PLETION DEADLINE FOR THE PROJECT WAS DECEMBER 31, 1971< A DEADLINE ESTABLISHED BY THE ILLINOIS COMMERCE COMMISSION AS PART OF A



RATE CASE.



     THE BABCOCK AND WILCOX PROCESS WAS GUARANTEED TO REMOVE 96 PERCENT OF THE FLY ASH AND 76 PERCENT OF THE SULFUR DIOXIDE. THESE



EFFICIENCIES WERE BASED ON A DuST  INLET LOADING  OF 1.355 GRAINS PER STANDARD CUBIC FOOT AT 70 F AND ON BURNING OF ILLINOIS COAL



CONTAINING H PERCENT SULFUR.



     THE WILL COUNTY POWER STATION IS LOCATED NEAR ROMEOVlLLEt ILLINOIS. THE PLANT HAS FOUR ELECTRIC POWER GENERATING UNITS WITH A



TOTAL RATED CAPACITY OF Il«t7 MW.   ONLY UNIT NO.  1 IS RETROFITTED WITH AN FGD SYSTEM.



     UNIT NO. i is A WET-BOTTOM COAL-FIRED BOILER PRODUCING 167 MW OF ELECTRICITY.  THE BOILER WAS MANUFACTURED BY BABCOCK AND



WILCOX AND WAS INSTALLED  IN 1955.   THE PLANT NOW BURNS A LOW-SULFUR (1.3 PERCENT) WESTERN COAL AND A HIGH-SULFUR  (4.0 PERCENT)



ILLINOIS COAL.



     THE WET LIMESTONE FGD SYSTEM  AT WILL COUNTY WAS PLACED IN SERVICE ON FEBRUARY 23, 1972.  THE SYSTEM CONSISTS OF TWO F60



MODULLS  (IDENTIFIED AS A  AND B)« LIMESTONE HANDLING AND MILLING FACILITIES, AND A SLUDGE TREATEMENT AND STABILIZATION UNIT.  A



PROCESS FLOW DIAGRAM OF THE FGO SYSTEM IS GIVEN  IN FIGURE 
-------
WILL COUNTY (CONTINUED)



SLUDGE FROM THE SYSTEM IS SENT TO A CLARIFICR.  THE OVERFLOW IS RETURNED TO THE PROCESS** THE UNDERFLOW IS STABILIZED BY MIXING



IT WITH LI PIE AND FLY ASH.  APPROXIMATELY 200 POUNDS OF LIME AND HOO POUNDS OF FLY ASH ARE USED PER TON OF DRY SOLIDS OF SLUDGE.



THE STABILIZED SLUDGE IS STABILIZED IN AND TRANSPORTED BY CONCRETE MIXING TRUCKS FOR ULTIMATE DISPOSAL IN AN OFF-SITE DISPOSAL



AREA.



PROBLEMS AND SOLUTIONS



     1972 - DEMISTER PLUGGING WAS A CONSTANT PROBLEM,MAINLY BECAUSE OF HEAVY LIMESTONE ACCUMULATIONS ON THE BOTTOM Of THE DEMISTER



AND PARTLY BECAUSE OF LOW WASHWATER PRESSURE CAUSED BY LEAKS IN THE POND KETURN BYPASS.  BECAUSE OF THESE PROBLEMS MODULES A AND B



WERE OUT OF SERVICE FOR SEVERAL DAYS EACH MONTH DURING MARCH, APRIL. JUNE. AND JULY 1972.  THE MODULES WERE ALSO OUT OF SERVICE



FROM SEPTEMBER 26 TO NOVEMBER 21* 1973* BECAUSE THE BOILER WAS DOWN.



     IN ORDER TO SOLVE THE DEMISTER PROBLEM* THE SLURRY NOZZLES WERE LOWERED AND THE SLURRY CIRCULATION SYSTEM WAS LEFT OUT OF



SERVICE TO KEEP THE DEMISTER CLEAN.  SINCE THE SITUATION DID NOT IMPROVE, THE DEMISTER ELEMENTS WERE HAND-WASHED.  THIS SOLVED THE



PROBLEM PARTIALLY* BUT CAUSED DIFFICULTY WITH THE VENTURI NOZZLES BECAUSE BROKEN ELEMENTS FROM THE DEMISTER GOT INTO THE SLURRY




SYSTEM.



     AT HIGH  GAS FLOW  RATES, THE REHEATER OF MODULE B VIBRATED EXCESSIVELY.  THEREFORE, MODULE B WAS TAKEN OUT OF SERVICE IN APRIL



TO ALLOW  REHEATER  MODIFICATIONS, WHICH  INCLUDED REBRACING OF THE REHEATER TUBES AND INSTALLATION OF A BAFFLE PLATE TO REDUCE THE




VIBRATIONS.



     OTHER REASONS FOR OUTAGES  WERE EROSION  AND PLUGGING OF SPRAY NOZZLES, INTERNAL AND EXTERNAL BUILDUP OF DEPOSITS ON VENTURI




NOZZLES,  CORROSION,  SULFITE  BLINDING  PROBLEMS, AND  FAN  VIBRATIONS.



     1973 -  DEMISTER  PLUGGING  CONTINUED.  FURTHERMORE,  THE OEMISTER ON MODULE B BROKE LOOSE FROM ITS MOUNTINGS AND THE RESULTANT



CARRYOVER OF  WASH-WATER  PLUGGED THE REHEATER.  THIS REHEATER  ALSO LEAKED  BECAUSE OF CHLORIDE PITTING CORROSION.  MODULE A WAS DOWN



FROM APRIL 24 TO MAY  2
-------
WILL COUNTY (CONTINUED)
MONTH OF JANUARY 197*.
     1975 - ENTERING 1975 NODULE A WAS OPERATIONAL AND NODULE B WAS STILL UNDERGOING MODIFICATION*  IN THE FIRST QUARTER OF 1975
THERE WERE EIGHT A-MODULE OUTAGES* ONLY ONE WAS A FORCED OUTAGE. DUE TO THE SPLITTING OF A SLURRY VENTURI SUPPLY HOSE.  MOBULE B
WAS RETURNED TO SERVICE ON MAY 20, 1975.  THE UTILITY DECIDED TO OPERATE THE SCRUBBER ON ILLINOIS HIGH-SULFUR COAL.  WHEN THIS
OPERATION BEGAN, A MULTITUDE OF PROBLEMS OCCURRED*  LOWER PARTICULATE REMOVAL EFFICIENCIES* HIGH SLURRY CARRYOVERS* DEMISTER
PLUGGING, REHEATER COIL FOULING AND LEAKS.  MODULE A WAS TAKEN OUT OF SERVICE IN MID-JUNE FOR THE REMAINDER OF 1975.  BY MID-
SEPTEMBER 1975 MODULE B WAS TAKEN OUT OF SERVICE OWING TO MASSIVE SCALING IN THE ABSORBER SYSTEM.  FINALLY* UNIT NO. 1 WAS SHUT
DOWN FOR OVERHAUL OF THE BOILER. TURBINE* AND SCRUBBER IN MID-OCTOBER* THIS OUTAGE LASTED MORE THAN «* MONTHS.
     PERFORMANCE FACTORS FOR EACH MODULE AND THE CORRESPONDING COMMENTS FOR THE REPORT PERIOD ARE PRESENTED IN THE FOLLOWING TABLE
                                                                93                                PEDCO ENVIRONMENTAL

-------
PERIOD             OPERABILITY («)
MONTH/YEAR       MODULE A   MODULE B
MAR. 72
APR. 72
MAY  72
JUN. 72
JUL. 72

AUG. 72
SEP. 72
OCT. 72
70
79
          35
32
          31
21
          30
              FGD SYSTEM OPERABILITY

              WILL COUNTY UNIT NO. 1


                        COMMENTS

MODULE A DOWN FOR REPAIR AND MODIFICATION OF DEMISTER WASH PIPING ASSEMBLY.

MODULE B WAS REMOVED  FROM SERVICE EVERY 2 OR 3 DAYS TO HAND-WASH THE DEMISTER. OTHER

PROBLEMS WERE VIBRATION OF KEHEATER TUBE BUNDLE, RAPID EROSION OF SCRUBBER SPRAY

NOZZLESt PLUGGING OF VENTURI NOZZLES.

MODULE A OUT OF SERVICE FOR 6 DAYS BECAUSE OF NEAR-RUPTURE OF A VENTURI PIPE

EXPANSION JOINT.  HEAVY BUILDUP OF SOLIDS ON OEMISTER.  MODULE B OUT OF SERVICE MOST

OF THE TIME FOR SIMILAR REPAIR OF VENTURI PIPE EXPANSION JOINT, AND FOR MODIFICATION

OF REHEATER UNIT AND DEMISTEK WASH SYSTEM.

A TWO WEEK OUTAGE OF MODULE B TO REBRACE THE REHEATER UNIT* TO INSTALL UNDERSPRAY

NOZZLES ON OEMISTERi AND TO INSTALL HEAVIER SCREENS IN THE SUMP.  REHEATER PLUGGING

CAUSED ADDITIONAL OUTAGES.

BOTH MODULES WERE OUT OF SERVICE OWING TO HIGH DIFFERENTIAL PRESSURE ACROSS THE

DEMISTERS. LEAKAGE OF POND RETURN BYPASS VALVE CAUSED DEMISTER PLUGGING.  ALSO

DURING THIS PERIOD. THE RUBBER LINING OF SCRUBBER A WAS REPAIRED.



PLUGGING OF VENTURI NOZZLES AND DEMISTER CAUSED SHUTDOWN OF MODULE A FOR 2 DAYS FOR

REPAIRS.  MODULE B WAS OUT OF SERVICE FOR 22 DAYS FOR CLEANING OF THE DEMISTER AND

REHEATER UNIT,  INSTALLATION OF OVERHEAD SPRAY NOZZLES, AND REPLACEMENT OF SECTIONS OF

THE OEMISTER.   THE BOILER WAS DOWN FOR TWODAYS FOR REPAIR OF THE GENERATOR.

BOILER DOWN SEPT. 1-5 BECAUSE OF NO DEMAND.  I.D. FAN PROBLEM CAUSED UNSTABLE OPERA-

TION OF THE BOILER MOST OF THE MONTH.  MODULE A WAS DOWN FOR MODIFICATION OF REHEATER

UNIT AND REPAIR OF RECIRCULATION TANK SCREENS.

BOILER AND SCRUBBERS WERE DOWN.  PRINCIPAL MODIFICATIONS INCLUDED INSTALLATION OF

REHEATEK «AFFLE PLATES TO DAMPEN VIBRATIONS AND INSTALLATION OF AN EXPERIMENTAL
                                                                                                  PEOCO ENVIRONMENTAL

-------
PERIOD
MONTH/YEAR
NOV. 72

DEC. 72



JAN. 73

FEB. 73



MAR. 73



APR. 73
  OPERABILITY (X)
MODULE A   MODULE B
OCT.  73
NOV.  73
DEC.  73
     0

    22




     0

    22




    65
     32
     51
 0

30



 0

2
-------
 PERIOD            OPERABILITY 
MONTH/YEAR       MODULE A   HOOULE  B
JAN. 74
FEB. 7*
MAR. 7
-------
 PERIOD
MONTH/YEAR

NOV. 74
DEC. 7H
JAN. 75
FEB. 75
  OPERABILITY 
-------
                                                     WILL  COUNTY UNIT  NO.  1  (CONTINUED)
 PERIOD    MODULE
MONTH/YEAR

MAR. 75        A
          SYSTEM PERFORMANCE FACTORS (K)
      AVAILABILITY  OPERABIHTY  RELIABILITY  UTILIZATION
                                      93
                                     81
APR. 75
           37
             
-------
                                                    WILL COUNTY UNIT NO. 1 (CONTINUED)
 PERIOD    MODULE
MONTH/YEAR
           SYSTEM PERFORMANCE FACTORS (X)
       AVAILABILITY   OPERABIL1TY   RELIABILITY   UTILIZATION
JUN. 75
A


B
6
-------
                                                     WILL COUNTY  UNIT NO.  1  (CONTINUED)
  PERIOD    MODULE
MONTH/YEAR
   SYSTEM PERFORMANCE FACTORS (XI
AVAILABILITY  OPERABILITY  RELIABILITY  UTILIZATION
AUG. 75
                  100
92
76
 SEP. 75
                               63
             63
OUT. 75
                 100
             26
                         COMMENTS
SULFUR COAL WAS BURNED DURING THE FIRST (3) WEEKS
AND HIGH SULFUR ILLINOIS COAL WAS BURNED DURING TH
THE LAST WEEK OF THE MONTH.
MODULE A REMAINED OUT OF SERVICE ALL MONTH. MODULE
B WAS SHUT DOWN SEVEN TIMES DURING THE MONTH, FOUR
OF WHICH WERE DUE TO »NO DEMAND.* HIGH SULFUR PILE
COAL WAS BURNED IN THE UNIT DURING THE MONTH,
RESULTING IN A SUBSTANTIAL INCREASE IN SLUDGE PRO-
DUCTION AND FORCING A 6-DAY. 10 HR/DAY, SLUDGE
DISPOSAL OPERATION.  SLUQGE STABILIZATION IS
CONTINUING.
MODULE A REMAINED OUT OF SERVICE ALL MONTH BECAUSE
OF DELAY ON THE NEW REHEATER ORDER.  MODULE B WAS
DOWN THREE TIMES BECAUSE OF MASSIVE ABSORBER SCALE
DEMISTER AND 1.0. BOOSTER FAN CLEANING, BALANCING
I.D. BOOSTER FAN, AND PLUGGING OF ABSORBER PUMP
SCREEN.  TOTAL OUTAGE TIME WAS 238 HOURS, HO
MINUTES FOR CUEANOUT AND FAN BALANCING.  HIGH
SULFUR COAL WAS BURNED IN THE BOILER WHEN THE
SCRUBBER WAS IN THE GAS PATH.
ON OCTOBER 11• OVERHAUL BEGAN ON THE WILL COUNTY
UNIT NO. 1 BOILER, TURBINE,AND SCRUBBER. MODULE  B
EXPERIENCED TWO MINOR OUTAGES DURING THE 11-DAY
PERIOD PRIOR TO THE OVERHAUL.  MODULE A REMAINED
                                                                60
                                                                           PEDCO ENVIRONMENTAL

-------
                                                     WILL COUNTY UNIT NO. 1 (CONTINUED)
  PERIOD    NODULE
MONTH/YEAR
NOV. 75
            SYSTEM  PERFORMANCE  FACTORS  (X)
        AVAILABILITY   OPERABXLITY  RELIABILITY  UTILIZATION
     TURBINE«  BOILER,  AND  SCRUBBER  OVERHAUL
DEC. 75
     TURBINE. BOILER AND SCRUBBER OVERHAUL
JAN. 76

FEB. 76
MAR.  76
     TURBINE* BOILER AND SCRUBBER OVERHAUL

     TURBINE* BOILER AND SCRUBBER OVERHAUL
A

B
30

 9
45

20
21

 8
19

 8
                         COMMENTS

OUT OF SERVICE PENDING DELIVERY OF THE NEW RE-

HEATER

THE SCHEDULED OVERHAUL OF THE BOILER* TURBINE* AND

SCRUBBER MODULES CONTINUED*  MAJOR MAINTENANCE

AREAS INCLUDED MODULE REHEATERS* POND RETURN PUMP*

VENTURI SPRAY NOZZLES* VENTURI AND ABSORBER

MODULES* PUMP VALVES* AND SUMPS.

MODULE B REHEATER WAS RETURNED FROM MANUFACTURER

AFTER REPAIRS AND REVISIONS.  SCRUBBER REHEATERS

COULD BE INSTALLED AND OPERATING BY THE END OF

JANUARY.

THE UNIT REMAINED OUT OF SERVICE FOR COMPLETION OF

THE BOILER* TURBINE* AND SCRUBBER OVERHAUL THAT

BEGAN ON OCTOBER 11* 1975.  SYSTEM RESTART IS NOW

SCHEDULED FOR MID-MARCH 1976.

UNIT NO. i RETURNED TO SERVICE IN MARCH FOLLOWING

THE EXTENDED MAJOR BOILER* TURBINE AND SCRUBBER

OVERHAUL.  THE A-SIDE WAS PUT INTO THE GAS PATH

ON MARCH 22 AND REMAINED AVAILABLE FOR SERVICE THE

REST OF THE MONTH.  THE B-SIDE REMAINED OUT OF

SERVICE UNTIL MARCH 29 BECAUSE OF DELAYS  IN THE

INSTALLATION OF A REPAIRED REHEATER.  HIGH SULFUR

ILLINOIS WAS BURNED IN THE BOILER DURING  THE MONTH
                                                                                                  PEOCO ENVIRONMENTAL

-------
                                                     WILL COUNTY UNIT NO.  1  (CONTINUED)
  PERIOD    MODULE
MONTH/YEAR
    SYSTEM PERFORMANCE FACTORS 
AVAILABILITY  OPERABILITY  RELIABILITY  UTILIZATION
APR. 76
  A
  B
A X B*
23
51
20
«f9
20
                               20
                                                                   19
                                                                   19
 HAY   76
    87
                                         85
                                        76
                         COMMENTS
DURING THE MONTH OF APRIL THE A-SIDE INCURRED PUMP
LINER FAILURES WHEN AN ISOLATION VALVE BROKE AND
FELL INTO THE VENTURI RECYCLE PUMP. B-SIOE OUTAGES
DURING THE MONTH RESULTED FROM REHEATER TUBEBUNDLE
LEAKS* PLUGGED ABSORBER TANK SCREEN* AND VENTURI
PUMP LINER FAILURE.  HIGH SULFUR COAL (3.5 PERCENT
SULFUR) WAS BURNED IN THE BOILER THROUGHOUT THE
MONTH.  IN ADDITION! THE UTILITY INITIATED A
TESTING AND EVALUATION PROGRAM DURING THE MONTH.
THIS PROGRAM IS DESIGNED TO PROVIDE DATA AND
INFORMATION CONCERNING CHEMISTRY AND RELATED
OPERATING CHARACTERISTICS.
THE A-SIDE WAS DOWN THE ENTIRE MONTH AWAITING A
PARTS SHIPMENT (VENTURI PUMP LINERS).  MODULE B
ENCOUNTERED FOUR FORCED SCRUBBER OUTAGES.  THREE
OF THESE OUTAGES WERE MECHANICAL PROBLEMS* DUE
TO A VENTURI HOSE LEAK, PLUGGED ABSORBER TANK
SCREEN, AND A FOULED I.D. BOOSTER FAN.  HIGH
SULFUR  ILLINOIS COAL WAS BURNED IN THE BOILER
DURING  THE MONTH.  THE SLUDGE WAS STABILIZED WITH
LIME AND FLY ASH AND HAUuED TO AN OFF-SITE
DISPOSAL AREA.
                                                                                                  PEOCO  ENVIRONMENTAL

-------
                                                     WILL COUNTY UNIT NO. X (CONTINUED)
  PERIOD    MODULE
MONTH/YEAR
JUN. 76
            SYSTEM PERFORMANCE FACTORS (X)
        AVAILABILITY  OPERABILITY  RELIABILITY   UTILIZATION
A
B
A & B*
50
63

44
85
37
42
01

36
70
31
JUL. 76
A
B
20
86
 0
90
 0
64
 0
72
AUG. 76
A
B
A 1 B*
98
65

57
61
17
96
54

38
41
11
                         COMMENTS
SIDE-A WAS RETURNED TO SERVICE JUNE 9 FOLLOWING
THE INSTALLATION OF A NEW VENTURI PUMP LINER.
FOUR FORCED SCRUBBER OUTAGES WERE REPORTED-
TWO BECAUSE OF NO DEMAND, ONE FOR A BYPASS-
DAMPER FAILURE AND ONE FOR 1.0. BOOSTER FAN
FOULING.  THE B-SIDE ENCOUNTERED SEVERAL FORCED
SCRUBBER OUTAGE - TWO DUE TO NO DEMAND AND
SEVERAL SHORT TRIPS BECAUSE OF SCALING AND
PLUGGING IN THE VENTURI TANK SCREEN.  HIGH SULFUR
ILLINOIS COAL WAS BURNED IN THE BOILER DURING
THE MONTH.  SLUDGE FIXATION AND HAULAWAY TO A
DISPOSAL SITE CONTINUED.
THE A-SIOE REMAINED OUT OF SERVICE THE ENTIRE
MONTH BECAUSE OF REPAIRS TO A DAMAGED ABSORBER
PUMP AND POND THICKENER SLUDGE OVERLOADING.  THE
B-SIDE ENCOUNTERED FOUR FORCED SCRUBBER OUTAGES*
TWICE FOR NO DEMAND* ONCE TO BALANCE THE I.D.
BOOSTER FANS, AND ONCE TO WASH THE I.D. BOOSTER
FANS.
THE A-SIOE REMAINED OUT OF SERVICE SO PERCENT OF
OF THE TIME DURING THE MONTH TO AVOID POND
THICKENER OVERLOADING.  FOUR SCRUBBER OUTAGES
WERE REPORTED*  ONE BECAUSE OF NO DEMAND AND THREE
BECAUSE OF MINOR PROBLEMS.  THE B-SIDE ENCOUNTERED
                                                                                                  PEOCO ENVIRONMENTAL

-------
                                                     WILL  COUNTY  UNIT  NO.  1  (CONTINUED)
  PERIOD    MODULE
MONTH/YEAR
    SYSTEM PERFORMANCE FACTORS (X)
AVAILABILITY  OPERABILITY  RELIABILITY  UTILIZATION
SEP. 76
  A

  B

A & B*
H2

79
29

76

 5
25

7H
                                                                   60
                                                                                  COMMENTS

                                                         THREE NO-DEMAND OUTAGESt  TWO BECAUSE OF LOSS OF

                                                         CHEMICAL CONTROL. ONCE FOR FOULING AND ONCE FOR

                                                         SPENT SLURRY VALVE REPAIRS.  EXPERIMENTATION WITH

                                                         THE SYSTEM'S PROCESS CHEMISTRY,  BY LOWERING THE

                                                         PH SET POINT FROM 5.t TO  5.1, WAS CONDUCTED BY THE

                                                         UTILITY DURING THIS PERIOD.  THIS VARIATION IN

                                                         OPERATION WAS BELIEVED To HAVE CAUSED THE MAS-

                                                         SIVE GYPSUM SCALING IN BOTH MODULES WHICH OCCURRED

                                                         DURING THE PERIOD.  THE PH SET POINT WAS RETURNED

                                                         BACK TO THE 5.4 VALUE. HIGH SULFUR ILLINOIS COAL

                                                         WAS BURNED IN THE BOILER  DURING THE MONTH.  SLUDGE

                                                         STABILIZATION PRACTICES CONTINUED.

                                                         FIVE OUTAGE PERIODS WERE  REPORTED DURING THE MONTH

                                                         FOR THE A-SIOE, THREE OF  WHICH RESULTED FROM

                                                         FORCED SCRUBBER OUTAGES.   PROBLEMS WERE REPORTED

                                                         WITH LOW FLOW TRIPS IN THE VENTURI, NOZZLE FOULING

                                                         CLEANING AND INSPECTION OF THE RECIRCULATION TANK,

                                                         PUMPS AND VALVES, AND A PUMP MOTOR FAILURE.  THE

                                                         B-SIDE ENCOUNTERED FOUR FORCED SCRUBBER OUTAGES*

                                                         TWO BECAUSE OF SPENT SLURRY VALVE TROUBLE* ONE LOW

                                                         VENTURI FLOW TRIP AND ONCE BECAUSE OF LOSS OF

                                                         CHEMICAL CONTROL.  HIGH SULFUR ILLINOIS COAL

                                                         BURNING WAS CONTINUED IN  THE BOILER DURING THE

                                                         MONTH.
                                                                                                  PEDCO  ENVIRONMENTAL

-------
                                                     WILL COUNTY UNIT NO. 1 (CONTINUED)
  PERIOD    MODULE
MONTH/YEAR'
OCT. 76
MOV. 76
    SYSTEM PERFORMANCE FACTORS 
-------
                  TABLE S
PERFORMANCE DESCRIPTION FOR OPERATIONAL F60 SYSTEMS  12/76
 IDENTIFICATION NO.

 UTILITY NAME

 UNIT NAME

 UNIT LOCATION

 UNIT RATING

 FUEL CHARACTERISTICS

 F6D VENDOR

 PROCESS

 NEW OR RETROFIT

 START UP DATE

 FGO STATUS

 EFFICIENCY,
  PARTICULATES
 32

DETROIT EDISON

ST. CLAIR NO 6

BELLE RIVER MICHIGAN

 163 MW

COAL  3.7 PERCENT SULFUR

PEABODY ENGINEERING

LIMESTONE SCRUBBING

RETROFIT

 5/76

OPERATIONAL


99,7 PERCENT
   S02
 90  PERCENT
  WATEK  MAKE  UP
 OPEN LOOP 1.07GPM/MW
  SLUDGE DISPOSAL
  UNIT  COST
 OPERATIONAL
  EXPERIENCE
 UNSTABILIZED SLUUGE DISPOSED IN LINED POND
$92 / KW CAPITAL * 2.f MILLS/ KUH OPERATING
 REFER TO THE BACKGROUND INFORMATION SECTION IN TABLE 3 OF THIS REPORT.
 A  30-DAY VENDOR QUALIFICATION RUN AND A WEEK-LONG FINAL ACCEPTANCE TEST
 WERE  SUCCESSFULLY COMPLETED DURING THE SPRING OF 1976. THE UTILITY IS
 NOW IN  THE  PROCESS OF  CONDUCTING A MINIMUM TWO-MONTH INTERNAL DEMONSTRA-
 TION  PROGRAM DURING WHICH  THE. SCRUBBERS WILL  OPERATE IN THE S02-REMOVAL
 MODE. THIS  PROGRAM IS  BEING CONDUCTED PRIMARILY BY PLANT PERSONNEL.
 FOLLOWING COMPLETION OF  THE S02  PROGRAM.  THE  VENTURI SCRUBBERS WILL
 REMAIN  IN THE FLUE GAS PATH,  OPERATING IN THE PARTICULATE-KEMOVAL  MODE.
                                                             66
                                                                         PEDCO  ENVIRONMENTAL

-------
                                                           BACKGROUND INFORMATION



                                                                 ON



                                                            ST. CLAIR NO. 6



     THE ST. CLAIR POWER PLANT OF THE DETROIT EDISON COMPANY IS LOCATED ON THE ST. CLAIR RIVER IN BELLE RIVER* MICHIGAN. APPROXI-



MATELY <»5 MILES NORTHEAST OF DOWNTOWN DETROIT.  THIS PLANT CONTAINS 7 FOSSIL-FUEL-FIRED GENERATING UNITS WHICH HAVE A TOTAL NET



GENERATING CAPACITY OF 1775-MW.  UNIT NO. 6 IS A COAL-FIRED TWO-STAGE SUPERHEATER UNIT, CONTAINING TWO SEPARATE BOILER BOXES KNOWN



AS THE SOUTH BOILER AND THE NORTH BOILER.  THE TOTAL NE.T GENERATING CAPACITY OF THE NO. 6 UNIT IS 325 MW.  THE SUPERHEATER WAS



MANUFACTURED BY COMBUSTION ENGINEERING AND PLACED IN SERVICE IN 1961.  BOTH THE NORTH BOILER AND THE SOUTH BOILER ARE EQUIPPED



WITH EMISSION CONTROL SYSTEMS. THE UNIT CURRENTLY OPERATES AT EXCESS AIR RATES OF 115 TO 120 PERCENT.



     THE ST.CLAIR NO.6 BOILER FIRES EXCLUSIVELY A LOW SULFUR WESTERN SUBBITUMINOUS COAL ORIGINATING FROM THE DECKER COMPANY'S



OIETZ MINE LOCATED IN SOUTHERN MONTANA. THE AVERAGE CHARACTERISTICS OF THIS COAL ARE* HEAT CONTENT 9500 TO 9600 8TU/t_B*SULFUR CON-



TENT OF 0.3 TO 0.«* PERCENT* ASH CONTENT OF 4.0 PERCENT* AND A TOTAL MOISTURE CONTENT OF 22.0 TO 2H.O PERCENT.



     THE EMISSION CONTROL SYSTEM INSTALLED ON THE NORTH BOILER CONSISTS OF MECHANICAL COLLECTORS AND AN ELECTROSTATIC PRECIPITATOR



(ESP) INSTALLED UPSTREAM OF A WET SCRUBBING SYSTEM. THE MECHANICAL COLLECTORS AND ESP ARE PROVIDED FOR PRIMARY PARTICULATE CONTROL



THE WET SCRUBBING SYSTEM PROVIDES ADDITIONAL PARTICULATE REMOVAL  AND PRIMARY SULFUR DIOXIDE CONTROL.



     THE FLUE GAS DESULFURIZATION (FGD) CONSISTS OF TWO PEABODY-LURGI VENTURI SCRUBBER AND SPRAY TOWER ABSORBER MODULES WITH A



TOTAL FLUE GAS CAPACITY OF 193,500 ACFM AT 270 F.  THIS VOLUME IS EQUIVALENT TO APPROXIMATELY 50 PERCENT OF THE TOTAL FLUE GAS




FROM THE NO. 6 UNIT.  THE DESIGN FLOW RATE PER SCRUBBING TRAIN IS 246*700 ACFM AT 270 F.  FLUE GAS CAN BE BYPASSED AROUND THE



SCRUBBING SYSTEM.  6.6 MW OF ELECTRICAL POWER ARE CONSUMED BY THE SCRUBBING OPERATIONS.  THIS FGO SYSTEM IS AN EXPERIMENTAL



DEMONSTRATION UNIT DESIGNED AND INSTALLED BY PEABODY ENGINEERED SYSTEMS IN COOPERATION WITH THE DETROIT EDISON COMPANY.  EACH



SCRUBBING TRAIN WHICH ALSO INCLUDES A CLEAR WATER TRAY AND RADIAL VANE MIST ELIMINATOR. A COMMON RECYCLE TANK, INDUCED DRAFT FAN*



OIL-FIRED HOT-AIR-INJECTION REHEAT SYSTEM AND A 10.8-ACRE CLAY-LINED SETTLING POND.  DESIGN REMOVAL EFFICIENCY OF THIS EMISSION



CONTROL SYSTEM IS 99.7 PERCENT FOR PARTICULATES AND 90 PERCENT FOR SULFUR DIOXIDE BASED UPON HIGH SULFUR EASTERN COAL.  A DIAGRAM



OF ONE OF THE TWO PARALLEL SCRUBBING TRAINS IS PRESENTED IN FIGURE 5 OF APPENDIX C.
                                                                67                                PEOCO ENVIRONMENTAL

-------
                                                                F60 SYSTEM PERFORMANCE
                                                                 ST. CLAIR NO. 6
PERIOD                                                                COMMENTS
NOV. 7«t             INSTALLATION OF THE FGD SYSTEM WAS ESSENTIALLY COMPLETED BY THIS TIME.  A FAULTY INSTRUMENT PANEL WHICH WAS
DEC. 7 AND LASTED 27 HOURS.  THE RUN WAS TERMINATED BECAUSE OF A
                     REHEATER THERMOCOUPLE FAILURE.   A  SUBSEQUENT INSPECTION OF THE SCRUBBING SYSTEM REVEALED NO APPARENT ABNOR-
                     MALITIES OR MALFUNCTIONS.
 SEP.  75
OCT. 75             A  THIRD  HOT FLUE GAS RUN OF 
-------
                                                          F60 SYSTEM PERFORMANCE (CONTINUED)
                                                                     ST. CLAIR NO. 6
PERIOD                                                                COMMENTS
NOV. 75
DEC. 75             A FOURTH FLUE 6AS RUN OF 23 DAYS DURATION HAS TERMINATED DUE TO EXCESSIVE VIBRATION IN THE 1.0. BOOSTER FAN.
                    ONE OTHER SCRUBBER-RELATED OUTAGE OCCURRED WHEN THE PACKING OF ONE OF THE SCRUBBER RECIRCULATION PUMPS REQUIRE
                    MAINTENANCE.  S02 REMOVAL DURING THIS PERIOD WAS 90 PERCENT AND PARTICIPATE OUTLET LOADING WAS 0.1 LB/1000 LBS
                    OF FLUE GAS FOR 1 TO 3 PERCENT SULFUR COAL.
JAN. 76
FEB. 76
MAR. 76
APR. 76             THE 30-DAY VENDOR QUALIFICATION RUN AND FINAL ACCEPTANCE TESTS WERE COMPLETED BY MAY 29.  THE QUALIFICATION
MAY  76             RUN WAS CONDUCTED ON A *HANDS OFF* BASIS USING PLANT PERSONNEL EXCLUSIVELY.  THE SYSTEM WAS IN SERVICE 100
                    PERCENT OF THE TIME THE BOILER WAS OPERATIONAL.  THE FINAL ACCEPTANCE TEST CONSISTED OF SIX 4-HR. TEST RUNS
                    CONDUCTED IN THE SPACE OF ONE WEEK.  THE S02 REMOVAL EFFICIENCY FOR HIGH SULFUR COAL WAS 90.9 PERCENT.
                    PARTICULATE REMOVAL ALSO EXCEEDED DESIGN LEVELS.  NO MAJOR MECHANICAL OR CHEMICAL-RELATED PROBLEMS WERE
                    ENCOUNTERED.
JUN. 76
JUL. 76
AUG. 76             THE UTILITY IS NOW PREPARING TO CONDUCT A 2 MONTH MINIMUM INTERNAL SCRUBBER DEMONSTRATION PROGRAM TO ACQUIRE
                    OPERATING DATA AND INFORMATION.  FOLLOWING THE COMPLETION OF THIS PROGRAM THE BOILERS WILL FIRE LOW SULFUR
                    DECKER COAL (0.3 TO O.«f PERCENT) TO MEET S02 EMISSION REGULATIONS.  THE SCRUBBERS WILL CONTINUE TO OPERATE IN
                    THE PARTICULATE REMOVAL MODE.
SEP. 76             THE INTERNAL SQ2 SCRUBBING DEMONSTRATION PROGRAM COMMENCED ON OCTOBER 1«*.  THE SCRUBBERS OPERATED CONTINUOUSLY
OCT. 76             FOR 10 DAYS.  OPERATION WAS INTERRUPTED BY A FORCED SCRUBBER OUTAGE RESULTING FROM SCALE AND SOLIDS CARRYOVER
                    FROM THE WASH TRAY AND MIST ELIMINATOR TO THE SCRUBBER I.D. BOOSTER FAN ASSEMBLYt CAUSING VIBRATION AND
                    BALANCE PROBLEMS.  THE SCRUBBING SYSTEM WAS TAKEN OUT OF THE GAS PATH THE FAN WAS CLEANED OUT AND REBALANCED.
                    THE UTILITY PLANS TO MODIFY THE COMPONENT'S WASH SYSTEM FOR GREATER FLOW CAPABILITY AFTER COMPLETION

                                                                69                                PEOCO ENVIRONMENTAL

-------
                    OF THE  so2  SCRUBBING  PROGRAM.  OECO  ALSO  PLANS TO CONTINUE PARTICULATE SCRUBBING FOLLOWING THE



                    TERMINATION OF  THE  S02  PROGRAM BY UNCOUPLING THE SPRAY TOWERS AND MAINTAINING THE PEABODY-LURGI



                    VENTURI SCRUBBERS IN  THE  FLUE  GAS STREAM.  SOME  LIMESTONE MAY HAVE TO BE  ADDED TO THE PARTICULATE SCRUBBING



                    SOLUTION IN ORDER TO  PREVENT LOW PH SWINGS AND  MINIMIZE THE POSSIBILITY  OF  ACID CORROSION DAMAGE TO  THE



                    INTERNAL COMPONENTS.



NOV. 76             FOLLOWING THE COMPLETION  OF SAND BLASTING  OPERATIONS TO SCRUBBER'S  I.D.  BOOSTER FAN FOR REMOVAL OF SOLIDS



                    BUILD UP, OPERATIONS  RESUMED ON NOVEMBER 7 AND  CONTINUED THROUGHOUT THE  MONTH. THE SYSTEM'S AVAILABILITY



                    INDEX FOR THE MONTH WAS 60 PERCENT, THE  MAJORITY OF THE OUTAGE  TIME WAS  CONSUMED PROCURING SAND BLASTING



                    SERVICES.  THE  OPERATION  ITSELF REQUIRED ONLY B HOURS.



DEC. 76             THE S02 DEMONSTRATION PROGRAM  CONTINUED  THROUGHOUT DECEMBER. THE SYSTEMS'S  AVAILABILITY INDEX FOR THE  PERIOD



                    WAS 51  PERCENT.  SCRUBBER  OUTAGES RESULTED  FROM  MALFUNCTIONS OF  THE  LIMESTONE FEEDER, THE DENSE SLURRY  TRAVERSE



                    PUMP, THE DENSE SLURRY  TANK AGITATORS* AND PLUGGING OF THE PH SAMPLE LINE,
                                                                70                                 PEDCO  ENVIRONMENTAL

-------
                  TABLE 3
PERFORMANCE DESCRIPTION FOR OPERATIONAL FGO SYSTEMS  12/76
 IDENTIFICATION NO.

 UTILITY NAME

 UNIT NAME

 UNIT LOCATION

 UNIT RATING
  33

DUQUESNE LIGHT

ELRAMA POWER  STATION

ELRAMA PENNSYLVANIA

  510  MW
 FUEL CHARACTERISTICS  COAL  1.0 - 2.8 PERCENT SULFUR
 FGO VENDOR

 PROCESS

 NEW OR RETROFIT

 START UP DATE

 FGD STATUS

 EFFICIENCY,
  PARTICULATES
 CHEMICO

 LIME SCRUBBING

 RETROFIT

 10/75

 OPERATIONAL
  S02
 83 PERCENT FOR 2X SULFUR COAL
 WATER HAKE UP
 OPEN LOOP
 SLUDGE DISPOSAL
  STABILIZED SLUDGE DISPOSED IN  UNLINED POND
 UNIT COST
S93/KW CAPITAL * 6.0 MILLS/KWHOPERATING COSTS(BOTH STATIONS)
 OPERATIONAL
  EXPERIENCE
 REFER TO THE BACKGROUND INFORMATION SECTION  IN TABLE 3 OF THIS  REPORT.
 THIS SCRUBBING SYSTEM,WHICH CONSISTS OF FIVE SINGLE-STAGE MODULES,WAS
 INITIALLY PLACED IN SERVICE OCTOBER 26,1975. INITIAL OPERATION  PROCEEDED
 WITH FLUE GAS FROM ONE BOILER BEING TREATED  BY FIVE SCRUBBING VESSELS.
 DURING THE REPORT PERIOD OPERATIONS PROCEEDED WITH TWO BOILERS  COUPLED
 INTO THE 5-MODULE SCRUBBING SYSTEM.-ONt SINGLE-STAGE SCRUBBING  MODULE
 OPERATED WITH TWO RUBBER-LINED RECYCLE PUMPS IN SERVICE.  THE SCRUBBING
 WASTES ARE CHEMICALLY FIXATED BY THE IUCS METHOD AND LANDFILLED.
                                                                                               PEOCO ENVIRONMENTAL

-------
                                                           BACKGROUND INFORMATION



                                                                 ON



                                                            ELRAMA POWER STATION



     DUOUESNE LIGHT COMPANY.  AN INVESTOR-OWNED ELECTRIC UTILITY, SERVES ABOUT ONE-HALF MILLION CUSTOMERS IN SOUTHWESTERN



PENNSYLVANIA AND HAS A NET GENERATING CAPABILITY OF APPROXIMATELY 2500 MW.  THIS CAPABILITY IS GENERATED BY COMBUSTION TURBINES IN



SIMPLE AND COMBINED-CYCLE MODES, BY NUCLEAR PLANTS, AND BY COAL-FIRED POWER STATIONS.  THE COMPANY IS SOLE OWNER AND OPERATOR OF



THREE COAL-FIRED STATIONS, TWO OF WHICH HAVE BEEN RETROFITTED WITH WET SCRUBBERS USING LIME AS A REAGENT. .



     THE SCRUBBER FACILITY AT THE 
-------
PERIOD
OCT. 75
  TO
JAN. 76
FEB. 76
MAR. 76
APR. 76
HAY  76
JUN. 76
JUL. 76
AUG. 76
    OPERATING HOURS
BOILER            SCRUBBER VESSELS
             1169  1508   976   838
SEP. 76
ELRAMA POliER STATION
                               COMMENTS
 ONE BOILER WAS CONNECTED TO THE SCRUBBER SYSTEM ON OCTOBER 26t 1975.
 A SECOND BOILER WAS CONNECTED ON FEBRUARY 4« 1976.  FOUR OF THE
 SCRUBBER VESSELS HAVE BEEN IN SERVICE IN VARIOUS COMBINATIONS.  THE
 SERVICE HOURS TO JANUARY 31t 1974 ARE POSTED IN THE ACCOMPANYING
 TABLE.  THE FIFTH VESSEL HAS NOT BEEN IN SERVICE BECAUSE IT IS BEING
 REVISED FOR TRIAL INSTALLATION OF RUBBER-LINED RECYCLE PUMPS.
 THE SYSTEM OPERATED DURING THE REPORT PERIOD WITH 2 BOILERS COUPLED
 INTO THE SCRUBBING SYSTEM.  REVISIONS TO THE FIFTH SCRUBBING VESSEL
 HAVE BEEN COMPLETED AND OPERATIONS ARE PROCEEDING WITH TWO RUBBER-
 LINED RECYCLE PUMPS.
 THE SYSTEM IS STILL OPERATING WITH TWO BOILERS COUPLED INTO THE
 SCRUBBING SYSTEM.  THE FIFTH SCRUBBING VESSEL WAS TAKEN OUT OF SERVICE
 FOR REPAIRS AND MODIFICATIONS REQUIRED FOR THE RUBBER-LINED RECYCLE
 PUMPS.  THE UTILITY IS CURRENTLY CONDUCTING A PERFORMANCE TEST ON
 THE SCRUBBING SYSTEM IN THE TWO BOILER OPERATION MODE.  THE IUCS
 SLUDGE FIXATION METHOD IS STILL CONTINUING AT THIS FACILITY.
 THE FIFTH SCRUBBING VESSEL EMPLOYING TWO RUBBER-LINED RECYCLE PUMPS
 WAS OPERATIONAL FOR A SHORT PERIOD OF TIME DURING THE REPORTING
 MONTHS.  TWO BOILERS REMAIN COUPLED INTO THE SCRUBBING SYSTEM.  THE
 CONSTRUCTION OF ADDITIONAL EQUIPMENT AT THIS FACILITY IS CONTINUING*
 ADDITIONAL LIME STORAGE SILOS AND A THICKENER WILL BE REQUIRED
 FOR FULL SCALE OPERATION.  THE UTILITY HAS SIGNED A LETTER OF INTENT
 WITH IUCS FOR A LONG-TERM SLUDGE FIXATION SYSTEM.  HIGH CALCIUM LIME
 IS STILL BEING EMPLOYED IN THE SCRUBBING SYSTEM.
 OPERATIONS AT THIS STATION DURING THE REPORT PERIOD PROCEEDED WITH
                                                                73
                                                                                   PEDCO ENVIRONMENTAL

-------
PERIOD
OCT. 76
BOILER            SCRUBBER VESSELS
    OPERATING HOURS
 NOV. 76
 DEC. 76
ELRAMA POWER STATION (CONTINUED)
                               COMMENTS
                                             TWO BOILERS COUPLED INTO THE 5-HODULE SCRUBBING SYSTEM.  THE STH
                                             SCRUBBING VESSEL WAS OPERATIONAL DURING THE REPORT PERIOD WITH THE
                                             RUBBER-LINED RECYCLE PUMPS IN SERVICE.  TESTS WERE CONDUCTED DURING
                                             THE PERIOD TO DETERMINE PARTICULATE AND «02 REMOVAL EFFICIENCIES.   S02
                                             REMOVAL EFFICIENCY WAS 50 PERCENT.  PARTICULATE EMISSIONS WERE BEING
                                             REDUCED WELL BELOW THE 0.1 LB/MM BTU STANDARD (ACTUAL RESULTS*  O.OH
                                             LB/MM BTU).  THESE RESULTS WEKC BASED ON 2 BOILERS COUPLED INTO THE 5
                                             SCRUBBING MODULES WHILE BURNING MEDIUM SULFUK U.O TO 2.6 PERCENT)
                                             COAL.  THE MECHANICAL COLLECTORS AND ESP'S WERE IN SERVICE DURING
                                             THE TESTS.  OPERATIONS ARE STILL PROCEEDING ON AN OPEN-WATER-LOOP
                                             BASIS.  PART OF THE THICKENER OVERFLOW IS STILL BEING DIVERTED TO THE
                                             ASH POND AND NOT RECYCLED BACK TO THE PROCESS,  BECAUSE BOTH THE
                                             BEAVER VALLEY AND BRUCE MANSFIELD STATIONS ARE FULLY OPERATIONAL,
                                             THIS STATION HAS BEEN RELEGATED TO PEAK LOAD OPERATIONS.  GENERAL LOAD
                                             OPERATIONS ARE FULL LOAD CAPACITY IN THE DAYTIME AND 50 TO 60 PERCENT
                                             LOAD REDUCTION AT NIGHT.
                                              THE SCRUBBER REMAINED IN SERVICE THROUGHOUT THE RPPORT PERIOD WITH
                                              TWO BOILERS COUPLED INTO THE SCRUBBING SYSTEM. RECYCLE PUMP EVALUA-
                                              TION  IS   BEING CONDUCTED BY THE UTILITY AT BOTH THE PHILLIPS AND
                                              ELRAMA STATIONS. OBSERVATIONS OF THE RUBBER-LINED RECYCLE PUMPS
                                             INDICATE  SOME SEVERE ABRASION AND GOUGING HAVE OCCURRED AFTER 1000
                                             HOURS  OF  SREVICE TIME.
                                                                                                  PEDCO ENVIRONMENTAL

-------
                  TABLE 3
PERFORMANCE DESCRIPTION FOR OPERATIONAL F60 SYSTEMS  12/76
 IDENTIFICATION NO.

 UTILITY NAME

 UNIT NAME

 UNIT LOCATION

 UNIT RATING
  3
-------
                                                           BACKGROUND INFORMATION



                                                                     ON



                                                           PHILLIPS POWER STATION



     THE PHILLIPS POWER STATION IS LOCATED ON THE OHIO RIVER ABOUT 20 MILES NORTHWEST OF PITTSBURGH.  THE POWER STATION CONSISTS



OP SIX COAL-FIRED BOILERS HAVING A NET GENERATING CAPABILITY'OF 307 MW.  THE RESULTANT FLUE GASES ARE DISCHARGED TO A COMMON



HEADER. TO WHICH THE FGD MODULES ARE CONNECTED THROUGH ISOLATION VALVES.  THE BOILERS ARE CURRENTLY BURNING COAL WITH A HEATING



VALUE OF 11.350 BTU PER POUND AND SULFUR AND ASH CONTENTS OF 2.2 AND 18.2 PERCENT, RESPECTIVELY.



     THE FGD SYSTEM, WHICH SUPPLEMENTS THE EXISTING MECHANICAL AND ELECTROSTATIC DUST COLLECTORS, CONSISTS OF FOUR TRAINS OF WET



VENTURI-TYPE SCRUBBERS, INSTALLED AT A COST OF APPROXIMATELY S103/KW.  GIBBS & HILL,  INC.. WAS ENGAGED AS THE A-E FIRM FOR THE



ENTIRE PROJECT* BATTERY LIMITS OF THE CHEMICO CORPORATION ARE CONFINED TO THE SCRUBBERS AND ASSOCIATED PUMPS AND CONTROLS BETWEEN



THE INLET HOT GAS DUCT MANIFOLD AND THE EXIT WET GAS HEADER (INCLUDING THE REHEATER,  EXCLUDING THE NEW ID FANS>.



     THE FOUR TRAINS ARE LOCATED DOWNSTREAM OF EXISTING MECHANICAL COLLECTORS AND ESP'S INSTALLED IN SERIES ON EACH OF THE SIX



PULVERIZED-COAL-F1RED BOILERS. THREE OF THE TRAINS ARE SINGLE-STAGE VENTURI SCRUBBERS ORIGINALLY INTENDED FOR PARTICULATE REMOVAL.



THE FOURTH TRAIN IS A DUAL-STAGE VENTURI SCRUBBER-ABSORBER AND IS THE PROTOTYPE FOR DETERMINING THE FEASIBILITY OF TWO-STAGE



SCRUBBING FOR COMPLIANCE WITH SULFUR DIOXIDE EMISSION LIMITS. A DIAGRAM OF THE SCRUBBER-ABSORBER TRAIN INSTALLED AT THE PHILLIPS



STATION  IS PRESENTED  IN FIGURE 6 OF APPENDIX C.



      EACH TRAIN  IS  EQUIPPED WITH A NEW WET-TYPE ID FAN.  A NEW COMMON DUCT DIRECTS GAS STREAMS FROM AIR BOILERS TO THE SCRUBBER



SYSTEM.  WHERE  THEY  CAN BE SENT TO ANY OR ALL OF THE TRAINS.  THE SCRUBBED GAS IS EXHAUSTED THROUGH A COMMON DUCT AND AN OIL-FIRED



REHEATER TO  A  NEW  GROUND-SUPPORTED STACK,  WHICH CONTAINS AN INNER ACID-RESISTANT BRICK STACK.




      SLAKED  QUICKLIME IS  ADDED TO THE LOWER CONE OF EACH OF THE SCRUBBER VESSELS TO NEUTRALIZE THE RECIRCULATING LIQUOR, WHICH, IN



SINGLE-STAGE SCRUBBING WITH HIGH-CALCIUM LIME, REACTS  WITH APPROXIMATELY 50 PERCENT OF THE SULFUR DIOXIDE IN THE FLUE GAS.  A



LIQUOR BLEED FLOW  OF  APPROXIMATELY 
-------
PHILLIPS POWER STATION NCONTINUEO)



DROPLETS ARE REMOVED BEFORE THE 6AS LEAVES THE SCRUBBER.



     STARTUP OF A PORTION OF THE PHILLIPS SCRUBBER SYSTEM BEGAN JULY 1973.  SEVERAL PROBLEMS THEN DEVELOPED IN THE FORM OF EROSION



OF FANS AND THE LIME FEED SYSTEM, CAUSING OUTAGES OF THE SCRUBBER SYSTEM.  AFTER AN EXTENDED OUTAGE* THE SCRUBBER SYSTEM WAS



RETURNED TO SERVICE IN MARCH 197t.  THE SYSTEM HAS BEEN OPERATING CONTINUOUSLY SINCE THAT TIME WITH VARIOUS NUMBERS OF BOILERS



CONNECTED TO THE SCRUBBER SYSTEM AND SCRUBBER TRAINS IN SERVICE.



     DETERMINATION OF THE AVAILABILITY OF THE PHILLIPS SYSTEM HAS BEEN DIFFICULT.  UNTIL ALL BOILERS WERE CONNECTED TO THE SCRUB*



BERS, THERE WAS AT LEAST ONE SPAKE TRAIN AND AS MUCH AS 100 PERCENT SPARE SCRUBBER CAPACITY.  THEREFORE , HAVING A TRAIN OUT OF



SERVICE FOR MAINTENANCE DID NOT REDUCE THE CAPABILITY OF THE SCRUBBER SYSTEM.  UNTIL ALL SIX BOILERS WERE CONNECTED. MEANINGFUL



AVAILABILITY FACTORS COULD NOT BE COMPUTED.  ON MARCH 17, 1975, THE SIXTH BOILER WAS CONNECTED* AND ALL FOUR SCRUBBER TRAINS WERE



REQUIRED TO BE IN SERVICE.  OPERATION IN THAT MODE CONTINUED UNTIL AUGUST «», 1975, WHEN THE NO. 6 BOILER WAS REMOVED FROM THE



SCRUBBER SYSTEM BECAUSE THE PH LEVEL COULD NOT BE MAINTAINED AND DEPOSITS BECAME UNMANAGEABLE TO THE POINT THAT SCRUBBER OUTAGES




WERE REDUCING GENERATING CAPABILITY OF THE STATION.
                                                                77                                PEDCO ENVIRONMENTAL

-------
                                                           PHILLIPS POWER STATION
                          OPERATING HOURS
                    BOILER                          SCRUBBER-ABSORBER
MONTH      1234      5      6      101    201    301    401                                COMMENTS
                                                                                FOURTH FGD TRAIN AND SIXTH BOILER WERE TIED IN ON
                                                                                MARCH 17,  1975. PARTICIPATE TESTS IN MAY SHOWED
JUL. 75   63    64«t  70S   349    60S    643     400    180    531    723       OUTLET LOADINGS OF 0.01 LB/MILLION BTU.  THE TWO-
                                                                                STAGE TRAIN HAS BEEN OUT OF SERVICE FROM JUNE 19
                                                                                FOR GENERAL CLEANING AND REPAIR OF A LEAK IN THE
                                                                                FIRST-STAGE SCRUBBER.
AUG. 75  354    701  454   457    517    445     478    682    323    319       SCRUBBER UNAVAILABILITY FORCED RETURNING BOILER
                                                                                NO, 6 TO THE SCRUBBER BYPASS GAS PATH TO PREVENT
                                                                                LOSS OF BOILER CAPACITY.  PLUGGING AND MAINTENANCE
                                                                                PROBLEMS HAVE BEEN ENCOUNTERED.  EVALUATION OF
                                                                                VARIOUS RECYCLE PUMPS IS CONTINUING.
 SEP. 75  463    287  669   503    672    525      57    561    685    536       IN OCTOBER 1975, PHILLIPS INITIATED THIOSORBIC
 OCT. 75  547    575  620   604    681    687      607   207    505    487       LIME SCRUBBING IN THEIR SINGLE-STAGE MODULES ON AN
                                                                                EXPERIMENTAL BASIS.  THE PURPOSE IS TO STUDY
                                                                                COMPLIANCE FEASIBILITY.  S02 REMOVAL EFFICIENCY*
                                                                                AND QUALITY OF THE SLUDGE GENERATED BY THE SINGLE-
                                                                                STAGE MODULES.
 NOV. 75    16    720  688     70    720    593     626    720      0     75       THE UTILITY CONCLUDED THE THIOSORBIC LIME TESTING
 DEC. 75  172    660  709      0    689    547     360    661    182    386       PROGRAM IN MID-DECEMBER. FOUR BOILERS WERE COUPLED
                                                                                TO THE SCRUBBING SYSTEM DURING THE RUN.  THE
                                                                                UTILITY IS NOW ANALYZING THE DATA GENERATED DURING
                                                                                THE TEST PROGRAM.  THE SCRUBBERS HAVE BEEN PUT
                                                                                BACK ON REGULAR LIME.  NO UNUSUAL PROBLEMS WERE
                                                                                ENCOUNTERED DURING THE TEST RUN.
JAN. 76  222    722  639     0    662    661     277    536    101    707       THE 2.5-MONTH TEST PROGRAM WITH THIOSORBIC LIME

                                                                78                                PEOCO ENVIRONMENTAL

-------
                                                     PHILLIPS POWER STATION (CONTINUED)

                          OPERATING HOURS
                    BOILER                          SCRUBBER-ABSORBER
MONTH      1234      5      6      101    201    301    401                                COMMENTS

                                                                                INCLUDED 1612 SERVICE HOURS ON ONE TRAIN AND 1309

                                                                                HOURS ON ANOTHER TRAIN.  RESULTS INDICATE THAT

                                                                                THE REQUIRED DEGREE OF So2 REMOVAL (83 PERCENT)

                                                                                CAN BE OBTAINED WITH AN MGO CONTENT OF 8-10

                                                                                PERCENT IN THE LIME WITH SINGLE-STAGE SCRUBBING.

FEB. 76  
-------
                                                    PHILLIPS POWER STATION  (CONTINUED)
MONTH
   BOILER
Z     3
                          OPERATING HOURS
  SCRUBBER-ABSORBER
101    201    301    101
JUL. 76

AUG. 76
                          COMMENTS

SCHEDULED TURBINE OVERHAUL TO UNIT NO. 6.  THE

SCRUBBING SYSTEM WAS SHUT DOWN ON JUNE 27 FOR A

SCHEDULED FOUR WEEK REPAIR PERIOD.  THE MAJORITY

OF THE WORK WILL BE CONCENTRATED ON THE STACK*

ASSOCIATED DUCTWORKt AND BOILER DAMPERS.  ALSO,

THE UTILITY IS PROCEEDING WITH THE INSTALLATION OF

3 ADDITIONAL LIME STORAGE SILOS AND A THIRD

THICKENER.

THE 4-WEEK SYSTEM OVERHAUL WAS COMPLETED JULY 25.

DURING THIS PERIOD, THE FOLLOWING REPAIRS AND

MODIFICATIONS WERE MADE*

     REPAIR OF THE TURNING VANES TO THE SCRUBBER

     DEMISTER.

     REPAIR OF THE EXPANSION JOINT SEAL WHERE THE

     DUCTWORK TIES INTO THE MAIN STACK.

     REPAIR OF STEEL BANDS AROUND INNER STACK

     STRUCTURE.

     OVERHAUL OF 1.0. FANS.

     REPAIR OF BOILER EXIT DAMPERS.

     REPAIR LEAKAGE OF  THE ACID-BRICK LINING  IN

     THE  MAIN STACK.

THE THREE ADDITIONAL LIME STORAGE SILOS AND THE

FOUNDATION FOR THE ADDITIONAL 75-FOOT DIAMETER

THICKENER HAVE BEEN INSTALLED.  THE UTILITY

HAS SIGNED A LETTER-OF-INTENT WITH IUCS FOR A
                                                                60
                                                                                 PEOCO ENVIRONMENTAL

-------
                                                          PHILLIPS POWER STATION (CONTINUED)
MONTH


SEP. 76
OCT. 76
                    BOILER
                 2     3
                          OPERATING HOURS
  SCRUBBER-ABSORBER
101    201    301    401
           TOTAL SCRUBBER HOURS* 23*274
           TOTAL BOILER HOURS* 63*642
           TOTAL SCRUBBER OUTA&E TIME* s*soo
           TOTAL SCRUBBER AVAILABILITY HOURS* 23*274
           AVERAGE HU LOAD/ SCRUBBER OPERATION HOUR* 243
           TOTAL OPERABILITT INDEX* 28 PERCENT
                               COMMENTS
     LONG-TERM SLUDGE TREATMENT SYSTEM.

     BOILER NOS. 2-6 WERE COUPLED INTO THE SCRUBBING
     SYSTEM.  BOILER NO. 1 IS DOWN FOR OVERHAUL AND
     REPAIRS.  THE IUCS INTERIM SLUDGE PROCESSING

     PLANT IS UNDER CONSTRUCTION AND WILL BE IN SERVICE
     BY DECEMBER 1976.  THE TEMPORARY FACILITIES WILL
     PROCESS THE THICKENER UNDERFLOW AND PONDED

     SLUDGE UNTIL THE POND IS DEPLETED OF SLUDGE AND

     THE PERMANENT FACILITY HAS BEEN INSTALLED.

     SCRUBBING OPERATIONS ARE STILL PROCEEDING IN AN

     OPEN-WATER-LOOP MODE WITH PART OF THE THICKENER

     OVERFLOW BEING DIVERTED TO THE ASH POND.

     BECAUSE BOTH THE BEAVER VALLEY AND BRUCE MANSFIELD

     STATIONS ARE FULLY OPERATIONAL* THIS STATION HAS

     BEEN RELEGATED TO PEAK LOAD OPERATIONS.  GENERAL

     LOAD OPERATIONS ARE FULL LOAD CAPACITY IN THE

     DAYTIME AND SO TO 67 PERCENT LOAD REDUCTION AT

     NIGHT.
THE FIGURES IN THE LEFT-HAND COLUMNS HAVE BEEN

COMPILED BY THE UTILITY FOR SYSTEM OPERATIONS FOR

THE PERIOD FOLLOWING START-UP IN JULY 1973 INCLUSIVE

TO OCTOBER 1976. THE TOTAL SCRUBBER HOURS VALUE IN-

CLUDE OPERATION TIME WHEN ONE OR MORE OF THE MODULES

WERE IN SERVICE. TOTAL BOILER AND UNAVAILITY VALUES

APPLY FOR ALL THE CORRESPONDING UNITS. THE TOTAL
                                                                61
                                                PEOCO ENVIRONMENTAL

-------
                                                         PHILLIPS POWER  STATION  (CONTINUED)
                    BOILER
                          OPERATING  HOURS
SCRUBBER-ABSORBER
NOV. 76



DEC. 76
                       SCRUBBER AVAILABILITY INDEX INCLUDES THE TIME WHEN



                       ONE OR MORE MODULES WERE AVAILABLE FOR SERVICE.



                      THE UTILITY REPORTS THAT BOILERS 2-6 REMAINED



                      COUPLED INTO THE SCRUBBING SYSTEM DURING THE REPORT



                      PERIOD. THE INTERIM UICS FIXATION FACILITY WAS IN-



                      STALLED AND COMMENCED OPERATIONS IN DECEMBER. THE



                      UTILITY REPORTS THAT THE VENTURI SCRUBBERS ARE STILL



                      DEVELOPING LARGE AMOUNTS OF SCALE ON THE INTERNALS.



                      RESULTING IN TWICE NORMAL PRESSURE DROPS.  THE RECYCLE



                      PUMP EVALUATION HAS BEEN IN PROGRESS. APPROXIMATELY



                      2500 TO 2800 HOURS OF OPERATION TIME HAVE BEEN AC-



                      CUMULATED ON THE VARIOUS UNITS WITH NO FAILURES OR



                      APPRECIABLE WEAR OBSERVED. THE ADDITIONAL OEWATERING



                      AND REAGENT PREPARATION EQUIPMENT IS NOW BEING IN-



                      STALLED. THE CONTRACT HAS BEEN AWARDED TO DRAVO TO




                      PROVIDE THIOSORBIC LIME FOR THIS SCRUBBING SYSTEM.
                                                                                                  PEDCO ENVIRONMENTAL

-------
                  TABLE 3
PERFORMANCE DESCRIPTION FOR OPERATIONAL F60 SYSTEMS  12/76
 IDENTIFICATION NO.
 UTILITY NAME
 UNIT NAME
 UNIT LOCATION
 UNIT RATING
 FUEL CHARACTERISTICS
 FGO VENDOR
 PROCESS
 NEW OR RETROFIT
 START UP DATE
 FGD STATUS
 EFFICIENCY,
  PARTICULATES
  36
 GENERAL MOTORS
 CHEVROLET PARMA  1234*
 PARMA  OHIO
   32 MM
 COAL   2.5  PERCENT  SULFUR
 KOCH/GENERAL  MOTORS
 DOUBLE ALKALI SCRUBBING
 RETROFIT
  3/7t
 OPERATIONAL

 60 PERCENT
  S02
 90 PERCENT
 WATER MAKE UP
 CLOSED LOOP
 SLUDGE DISPOSAL
 UNSTABILIZED SLUDGE DISPOSED IN UNLINED POND
 UNIT COST
S3.2 MILLION CAPITAL * S11.70 PER TON OF COAL ANNUALIZEO
 OPERATIONAL
  EXPERIENCE
 REFER TO BACKGROUND INFORMATION SECTION IN TABLE 3 OF THIS REPORT.
 THE EMISSION CONTROL SYSTEM FOR THESE f-COAL FIRED STOKER BOILERS
 CONSISTS OF MECHANICAL COLLECTORS INSTALLED UPSTREAM OF A DILUTE DOUBLE
 ALKALI SCRUBBING SYSTEM. THE FGD SYSTEM HAS BEEN IN SERVICE SINCE MARCH
 197H. SYSTEM OPERABILITY INDEX VALUES FOR THE MONTHS OF NOVEMBER AND
 DECEMBER WERE 60 PERCENT AND 22 PERCENT, RESPECTIVELY. THE ANNUAL
 SYSTEM OPERABILITY INDEX VALUE FOR 1976 AVERAGED 6<* PERCENT.
                                                                                               PEOCO ENVIRONMENTAL

-------
                                                            BACKGROUND INFORMATION
                                                                     ON
                                                       THE CHEVROLET PARMA STEAM PLANT
     THE CHEVROLET PARMA PLANT OF GENERAL MOTORS IS LOCATED NEAR  CLEVELANDt  OHIO.  THE PLANT HAS FOUR SPREADER-STOKER BOILERS
FIRED BY TRAVELING GRATES. CAPABLE OF PRODUCING A TOTAL OF 320,000 LB/HR OF STEAM OR APPROXIMATELY 32 MU OF EQUIVALENT ELECTRICAL
CAPACITY.  THE COAL FIRED IN THESE UNITS ORIGINATES PRIMARILY FROM THE SOUTHEASTERN PORTION OF OHIO AND HAS THE FOLLOWING AVERAGE
CHARACTERISTICS*  HEAT CONTENT OF XI,300 TO 13,900 BTU/LB* SULFUR CONTENT OF  1.7 TO 2.7 PERCENT*  ASH CONTENT OF 6.a TO m.6
PERCENT* AND A TOTAL MOISTURE CONTENT OF 0.9 TO 7.8 PERCENT.
     THE POWER BOILERS HAVE BEEN FITTED WITH AN EMISSION CONTROL SYSTEM CONSISTING OF MECHANICAL COLLECTORS UPSTREAM OF A DILUTE
DOUBLE ALKALI SCRUBBING SYSTEM.  THE FGD SYSTEM SCRUBBING MODULES WERE SUPPLIED BY KOCH ENGINEERING.  INSTALLATION WAS COMPLETED
ON FEBRUARY 26, 197t.  THE SYSTEM CONSISTS OF FOUR SCRUBBERS OPERATING IN PARALLEL.  EACH SCRUBBER CONTAINS THREE BUBBLE-CAP
ABSORPTION TRAYS AND A MESH MIST ELIMINATOR.
     THE SULFUR DIOXIDE CONTAINED IN THE BOILER FLUE GAS IS ABSORBED BY A REGENERATED CAUSTIC SOLUTION (0.1 MOLAR NAOH), FORMING A
SOLUTION OF  SOLUBLE SODIUM SALTS.  THE SPENT CAUSTIC IS THEN REGENERATED BY REACTING THE SODIUM SALT SOLUTION WITH SLAKED LIME,
RESULTING  IN THE FORMATION OF CALCIUM SULFlTE AND SULFATE SOLIDS, WHICH ARE SEPARATED OUT OF THE SOLUTION.  NEXT, SODA ASH IS
AODED  TO THE SOLUTION  IN  ORDER TO MAKE UP FOR SODIUM LOSSES AND MINIMIZE THE  SCALE POTENTIAL FROM THE CALCIUM WHICH REMAINS IN
SOLUTION.   THE REGENERATED  CAUSTIC FORMEU  IS THEN RECYCLED BACK TO THE SCRUBBER FOR ADDITIONAL SULFUR DIOXIDE REMOVAL.  THE
CALCIUM SALT AND  FLY  ASH  SLUDGE  WHICH RESULTS  IS DEWATERED AND HAULED AWAY BY TRUCK TO AN OFF-SITE LANDFILL.
PROBLEMS 'AND SOLUTIONS
      THE SYSTEM WAs STARTED UP ON  FEBRUARY 26,  197t AND  BY APRIL  31  IT HAD OPERATED FOR 62
-------
CHEVROLET PARMA (CONTINUED>



SIGN OR ABRASION IN THE PUMPS OR PIPING.



     THE SYSTEM WAS SHUT DOWN FROM MAY 1 TO MAY 28f 1974* BECAUSE OF UNEXPECTED BUILDUP OF SOLIDS IN THE CLARIFIERt WITH SUBSE-



QUENT OVERFLOW INTO THE SCRUBBER.  THE PROBLEM WAS SOLVED BY 1) USING A POLYMERIC FLOCCULATION AGENT TO ATTAIN BETTER SETTLING AND



2) WITHDRAWING SLUDGE FROM THE CLARIFIER AT MORE FREQUENT INTERVALS.  SYSTEM AVAILABILITY TO THE BOILER WAS 67 PERCENT IN APRIL



197«H LESS THAN 10 PERCENT IN MAYt AND 100 PERCENT IN JUNE, JULY. AND AUGUST AFTER THE SYSTEM WAS RESTARTED.  PLUGGING BY GYPSUM



DEPOSITS IN THE OVERFLOW LINE BETWEEN THE CLARIFIERS AND IN THE LINE FROM CLARIFIER NO. 2 TO THE MIX TANKS WAS CORRECTED BY



RELOCATING A CHEMICAL FEED LINE AND REPLACING SOME PIPING.  THE SYSTEM WAS DOWN THROUGHOUT JULY AND AUGUST FOR REPLACEMENT OF



GRAVITY FLOW LINES WITH AN OPEN FLUME THAT CAN BE EASILY CLEANED.  ADDITIONAL MODIFICATIONS TO THE DESIGN AND OPERATION OF THE FGD



SYSTEM HAVE CONTINUED.  THE OPERABILITY INOEX FOR THE FGD SYSTEM HAS INCREASED SIGNIFICANTLY THROUGHOUT THE COURSE OF 1976.  THE



MAJOR PROBLEM AND SOLUTION AREAS, PLUS MODIFICATIONS IMPLEMENTED TO THE SYSTEM ARE HIGHLIGHTED BELOW IN THE SYSTEM PERFORMANCE



TABLE.  A PROCESS FLOW DIAGRAM OF THE DOUBLE ALKALI UNIT IS PRESENTED IN FIGURE 7 OF APPENDIX C.
                                                                65                                PEOCO ENVIRONMENTAL

-------
                                                              CHEVROLET PARMA
MONTH

JUN. 75
   BOILER
1      2
                     OPERATION HOURS
F60 SYSTEM
  2      3
OPERABILITY (X>
234
JUL. 75

AUG. 75




SEP. 75

OCT. 75
NOV. 75

DEC. 75
        2331*
    16«»8*
79
        2135
    1250
59
               COMMENTS

RECENT OPERATION HAS BEEN INTERMITTENT.

TESTS HAVE BEEN CONDUCTED FOR ANALYSIS

OF PARTICIPATE LOADING AT THE BOILER

OUTLET.  THE SYSTEM WAS RESTARTED IN MAY

BUT WAS SHUT DOWN BECAUSE OF A PLUGGED

CHEMICAL FEED LINE TO CLARIFIER.  AFTER

RESTART* AROUND JUNE 10t THE SYSTEM WAS

SHUT DOWN BECAUSE OF SIMILAR PLUGGING IN

ANOTHER PART OF THE LINE.  UNIT RAN FOR

ABOUT 2 WEEKS IN JUNE.

FGD SYSTEM WAS DOWN IN JULY AND AUGUST

FOR REPLACEMENT OF GRAVITY FLOW LINES

WITH AN OPEN FLUME.

FGD SYSTEM RESTARTED SEPTEMBER 8t AND

OPERATED DURING THIS PERIOD AT AN

AVAILABILITY FACTOR OF 80 PERCENT.

  NOTE   THE FIGURES GIVEN FOR SEPTEMBER

  AND OCTOBER REPRESENT THE OPERATION

  HOURS FROM SEPTEMBER a TO NOVEMBER 9

THE FGD SYSTEM OPERATED DURING THE

REPORT PERIOD EXCEPT FOR A SCHEDULED

HOLIDAY SHUTDOWN FROM DECEMBER 23 TO

JANUARY Hi 1976.  BECAUSE OF PROBLEMS

WITH SOLIDS AND SOLIDS CARRYOVER* G.M.
                                                                                                  PEOCO ENVIRONMENTAL

-------
                                                               CHEVROLET PARMA
MONTH
BOILER
    2
                     OPERATION HOURS
                                            F60 SYSTEM
                                              Z      3
                              OPERABILITY  (*)
                              234
JAN. 76

FEB. 76
    2997
1196
NAR. 76
     1379
 240
APR.
     1064
 647
78
MAY  76
JUN. 76
     1149
     924
1042
 616
91



86


87
               COMMENTS

CONDUCTED STREAM TESTS DURING DECEMBER

 TO DETERMINE WHETHER SOLIDS CARRYOVER

IS DUE TO A HIGH SOLIDS RECIRCULATION

RATE.  THE FGD SYSTEM WAS DOWN MOST OF

DECEMBER BECAUSE OF THESE TESTS* WHICH

CAUSED THE LOW OPERABILITY FACTOR.

G.M. HAS FOUND SOLIDS CONCENTRATION IN

THE CLARIFIER TOO HIGH FOR EFFICIENT

SYSTEM OPERATION.A.D.LITTLE IS SCHEDULED

TO CONDUCT TESTS ON THE SYSTEM IN APRIL

AS PART OF AN EPA EVALUTATlON PROGRAM.

THE LOW OPERABILITY INDEX DURING THE

MONTH OF MARCH RESULTED FROM EXTENSIVE

MODIFICATIONS PERFORMED ON THE SYSTEM BY

6.M.  DURING THIS PERIOD THE SCRUBBER

BLOWDOWN AND SCRUBBER FLOW INDICATION

SYSTEM WAS REVISED.

FROM APRIL 19 TO THE END OF THE MONTH

THE SYSTEM WAS OPERABLE 100X.  DURING

THIS PERIOD ALL SYSTEM MODIFICATIONS

WERE COMPLETEP. AND ALL MAJOR PROBLEM

AREAS CORRECTED.

  NO MAJOR PROBLEMS WERE ENCOUNTERED

  DURING THE REPORTING PERIOD.

  ONE SYSTEM UPSET OCCURRED DURING THE


        PCDCO ENVIRONMENTAL

-------
                                                             CHEVROLET PARMA  (CONTINUED)

                     OPERATION HOURS
              BOILER                        F6D  SYSTEM                 OPERABILITY  («)
MONTH      12      3      
-------
                                                              CHEVROLET PARMA (CONTINUED)

                     OPERATION HOURS
              BOILER                        F60 SYSTEM                 OPERABILITY (X)
MONTH      123H1231123H                     COMMENTS

                                                                                     INITIAL PART OF THE MONTH.   A NUMBER OF

                                                                                     PROBLEMS WERE ENCOUNTERED*  FORCING A SHUT-

                                                                                     DOWN THROUGHOUT THE REMAINDER OF THE MONTH,

                                                                                     THESE INCLUDED*

                                                                                          SOLIDS DEPOSITION AND PLUGGING OF THE

                                                                                          CHEMICAL TANKS AND REACTORS. REQUIRING

                                                                                          SHUTDOWN AND CLEANOUT.

                                                                                          AGITATOR PROBLEMS.

                                                                                          BOILER PROBLEMS.

                                                                                          REPLACEMENT OF DEMISTER PADS.

OCT. 76          117*                   73*                     63                   THE SYSTEM WAS RETURNED TO SERVICE THE SECOND

                                                                                     WEEK IN OCTOBER*  TWO BOILERS AND THEIR

                                                                                     CORRESPONDING SCRUBBERS WERE PUT BACK IN THE

                                                                                     GAS STREAM.  PROBLEMS ENCOUNTERED STEMMED

                                                                                     PRIMARILY FROM A MECHANICAL COLLECTOR MAL-

                                                                                     FUNCTION*RESULTING IN EXCESSIVE DUST LOADINGS

                                                                                     IN THE MODULES AND EVENTUALLY CAUSING WIDE-

                                                                                     SPREAD PLUGGING OF THE LOWER BUBBLE-CAPE

                                                                                     TRAYS.  SHUTDOWN AND CLEANOUT Op THE MODULES

                                                                                     PLUS REPAIRS TO THE MECHANICAL COLLECTOR WERE

                                                                                     REQUIRED.  SYSTEM RESTART OCCURRED NOVEMBER

                                                                                     6.  MAJOR MODIFICATIONS PERFORMED TO THE

                                                                                     DOUBLE ALKALI SYSTEM DURING THE PERIOD

                                                                                     INCLUDED*

                                                                                          INSTALLATION Op A GREAT LAKES PH MONITOR



                                                                69                                PEUCO ENVIRONMENTAL

-------
MONTH
   BOILER
1      2
                     OPERATION HOURS
    FGD SYSTEM
      2      3
                                                             CHEVROLET PARMA  (CONTINUED)
       OPERABILITY (X)
       23*
NOV. 76
DEC. 76
      1321
      1559
787
349
60
22
                         COMMENTS
          AND CONTROL UNIT FOR THE REGULATION OF
          LIME FEED TO THE REGENERATION REACTOR-
          CLARIFIER UNIT.  THIS UNIT EMPLOYS A
          DIGITAL READOUT AND IS SCHEDULED FOR
          OPERATION SOMETIME IN NOVEMBER.
          SUPERIOR CRYSTAL GROWTH OF THE CALCIUM
          SULFITE/SULFATE SALTS HAS RESULTED BY
          RUNNING A SEEDING LINE BACK TO THE
          REACTOR-CLAKIFIER UNIT.
THE FGO FIGURES REPORTED FOR THE MONTH OF
DECEMBER ARE SOMEWHAT DISTORTED BECAUSE UAW
PERSONNEL CAN ONLY OPERATE THE SYSTEM AND
THEREFORE THE SCRUBBERS COULD NOT BE OPERATED
DURING THE CHRISTMAS HOLIDAY PERIOD. DURING THE
LATTER PART OF NOVEMBER AND EARLY DECEMBER
PERIOD THE SCRUBBERS WERE TAKEN OUT OF THE FLUE
GAS PATH BECAUSE OF CONTINUED SOLIDS BUILD UP
IN THE MIX TANK. IN ADDITION, SOME PIPING AR-
RANGEMENTS WERE MODIFIED AND THE GEAR REDUCER
IN THE MIX TANK HAD TO BE REPLACED.
                                                                90
                                                                                       PEOCO  ENVIRONMENTAL

-------
                  TABLE 3
PERFORMANCE DESCRIPTION FOR OPERATIONAL F60 SYSTEMS  12/76
 IDENTIFICATION NO.

 UTILITY NAME

 UNIT NAME

 UNIT LOCATION

 UNIT RATING

 FUEL CHARACTERISTICS

 F6D VENDOR

 PROCESS

 NEW OR RETROFIT

 START UP DATE

 FGD STATUS

 EFFICIENCY,
  PARTICULATES


  S02
 37

GULF POWER CO.

SCHOLZ NOS. IB 4 28

CHATTAHOOCHEE FLORIDA

  23 MW

COAL 5.0  PERCENT SULFUR  (MAX)

CHIYODA  INTERNATIONAL

THOROUGHBRED  101

RETROFIT

  3/75

OPERATIONAL


99.7 PERCENT


 90  PERCENT
  WATER MAKE UP
  SLUDGE DISPOSAL
 OPEN LOOP
 UNSTABILIZED SLUDGE DISPOSED IN DRY  GYPSUM POND
  UNIT COST
  OPERATIONAL
   EXPERIENCE
S3 MILLION CAPITAL COST
 REFER TO THE BACKGROUND INFORMATION SECTION  IN TABLE  3  OF  THIS REPORT.
 THIS PROTOTYPE DEMONSTRATION UNIT WAS  FIRST  PUT INTO  THE FLUE  GAS  PATH
 ON FEBRUARY 11.1976.  THE OPERABILITY INDEX FOR OPERATIONS  DURING 1975
 WAS 60 PERCENT. THE UNIT WAS IN SERVICE THROUGHOUT  THE  REPORT  MONTHS,
 ACHIEVING OPERABILITY INDEX VALUES OF  99.5 AND 99.6 PERCENT,RESPECTIVELY.
 THE ANNUAL AVERAGE OPERABILITY INDEX VALUE FOR 1976 OPERATIONS WAS 64
 PERCENTJFOR 9 MONTHS  OF OPERATION). THE PROTOTYPE FGD UNIT IS
 SCHEDULED TO CONTINUE OPERATIONS THROUGHOUT  THE COMING  YEAR.
                                                             91
                                                                         PEOCO ENVIRONMENTAL

-------
                                                                BACKGROUND INFORMATION



                                                                          ON



                                                            SCHOLZ UNITS 1 AND 2 - CHIYOOA



     THE SCHOLZ POWER PLANT IS LOCATED IN CHATTAHOOCHEE, FLORIDA*  ABOUT SO MILES WEST OF TALLAHASSEE.  THE F6D SYSTEM WAS DESIGNED



BY CHIYOOA INTERNATIONAL CORP. FOR TESTING AND PROCESS DEMONSTRATION ON A COAL-FIRED APPLICATION.  THE PROCESS IS USED IN JAPAN



EXCLUSIVELY ON OIL-FIRED AND GAS-FIRED BOILERS, AND TAIL GAS FROM  CLAUS UNITS.



     THE SYSTEM AT SCHOLZ CAN HANDLE ONE-HALF THE LOAD (53,000 SCFM) FROM EITHER OF THE 
-------
                                                         SCHOLZ IB AND 2B - CHIYODA
         TOTAL
MONTH    HOURS

FEB. 75    672
APR. 75    720
HAY  75    744
JUN. 75    720
JUt. 75    744
AUG. 75    744
SEP. 75    720
OCT. 75    744
NOV. 75    720
  UNIT OPERATING HOURS
BOILER    FGO SYSTEM
   672
   720        200
   744        100
             FGO  SYSTEM PERFORMANCE  (X)
           OPERABILITY     UTILIZATION
                 28
                 13
                26
                13
   685
   744
685
624
100
 84
 95
 84
   720
  0
337
 46
 46
   744
   720
744
720
100
100
000
100
                       COMMENTS
THIS IS A PILOT PLANT SIZE DEMONSTRATION UNIT.
1973.  INITIAL SHAKEDOWN AND DEBUGGING OPERATIONS
COMMENCED ON FEBRUARY 11, 1975.  PROBLEMS
ENCOUNTERED INCLUDED CRACKS IN THE FRP LINING AT
THE OXIDIZING TOWER.  STARTUP OCCURRED IN MARCH
1975.  AFTER INITIAL OPERATION FOR BREAK-IN TESTS,
THE UNIT WAS SHUT DOWN FOR INTERNAL INSPECTION.
RELIABILITY TESTS THEN FOLLOWED IN JULY 1975.
CHEMICAL PERFORMANCE WAS SATISFACTORY.  EMISSION
TESTS HAVE NOT BEEN PERFORMED.  SOME PUMP AND
INSTRUMENT FAILURES HAVE OCCURRED.
A 100 PERCENT OPERABILITY FACTOR WAS REGISTERED
FOR THE MONTH OF JUNE.  DURING THE MONTH OF JULY
ONE CENTRIFUGE BECAME UNBALANCED, REQUIRING THE
SPARE TO BE PLACED IN SERVICE.
DURING THE MONTH OF AUGUST BOTH CENTRIFUGES BECAME
UNBALANCED REQUIRING A FORCED OUTAGE WHICH
EXTENDED TO MID-SEPTEMBER.  UNIT OPERATED AT A
95 PERCENT SQ2 REMOVAL EFFICIENCY DURING THIS
PERIOD.  GULF POWER IS ATTEMPTING TO UPGRADE THIS
VALUE TO A HIGHER EFFICIENCY LEVEL.
WASTE WATER DISCHARGE FROM THIS UNIT STILL A
PROBLEM AREA.
OUTAGE TIME WAS LESS THAN ONE HOUR DURING NOVEMBER
                                                                93
                                                                               PEOCO ENVIRONMENTAL

-------
                                                   SCHOLZ  IB  AND 2B - CHIYOOA  (CONTINUED)
MONTH
TOTAL
HOURS
DEC. 75
JAN. 76
FEB. 76
MAR. 76
APR. 76
MAY  76
JUN. 76
  696
  720
  UNIT OPERATING HOURS
BOILER    FGD SYSTEM
             FGO SYSTEM PERFORMANCE (X)
           OPERABILITY    UTILIZATION
   680
   690
                        726

-------
                                                 SCHOLZ IB AND 2B - CHIYQOA (CONTINUED)
MONTH
TOTAL
HOURS
  UNIT OPERATING HOURS

BOILER    F60 SYSTEM
  F6D SYSTEM PERFORMANCE (X)
OPERABILITY    UTILIZATION
JUL. 76

AUG. 76
                        192
                               66
                     66
                       COMMENTS

THE REPORT PERIOD.  SYSTEM RESTART IS

SCHEDULED FOR THE END OF JULY.

THE PROTOTYPE UNIT REMAINED OUT OF SERVICE

MAY. JUNE AND JULY TO REPAIR THE FIRE-DAMAGED

AREAS.  THE SYSTEM WAS PUT BACK IN OPERATION

IN AUGUST.  THE SYSTEM WAS AGAIN BROUGHT DOWN

DURING THE MONTH TO COMPLETE ADDITIONAL REPAIRS

WHICH WENT UNDETECTED DURING THE PREVIOUS

OUTAGE.  2
-------
                                                 SCHOL2  IB  AND 2B  -  CHIYOOA  (CONTINUED)
                     UNIT OPERATING HOURS
         TOTAL                                FGD SYSTEM PERFORMANCE (X)
MONTH    HOURS     BOILER    FGO SYSTEM  AVAILABILITY OPERABILITY     RELIABILITY  UTILIZATION          COMMENTS
SEP. 76    780     720        496           99           69             99           69       TOTAL FORCED OUTAGE TIME DURING
                                                                                              THE MONTH AMOUNTED TO 5.1 HOURS.
OCT. 76    744     744        357           70           48             62           48       TOTAL DOWN TIME DURING THE MONTH
                                                                                              AMOUNTED TO 386.9 HOURS.  OF THIS
                                                                                              TOTAL 1.1 HOUR WAS ATTRIBUTED To A
                                                                                              FORCED SCRUBBER OUTAGE* 218 HOURS
                                                                                              WAS REQUIRED TO REPAIR EXPECTED
                                                                                              DAMAGES INCURRED IN THE PRE
                                                                                              SCRUB3ER RESULTING FROM OPERA-
                                                                                              TIONS IN THE WATER SAVINGS PROGRAM.
                                                                                              SPECIFICALLY« THE LINING WAS
                                                                                              SUFFERING FROM EXTENSIVE CORROSION
                                                                                              DAMAGE BECAUSE OF HIGH ACID
                                                                                              CONCENTRATIONS WHICH DEVELOPED
                                                                                              IN THE PKESCRUBBER SCRUBBER SOLU-
                                                                                              TION.  THIS OUTAGE WAS SCHEDULED
                                                                                                FOR INSPECTION, REPAIR, AND
                                                                                                PROVIDE DESIGN DATA FOR FUTURE
                                                                                                UNITS. S02 REMOVAL EFFICIENCY
                                                                                                STILL RESIDES IN THE 85-95
                                                                                                PERCENT RANGE.
NOV. 76    720      720         717           99           99              99          99      A TOTAL OF THREE FORCED SCRUBBER
DEC. 76    744      744         741           99           99               99           99     OUTAGE TIME TOTALLING 6.5 MRS WAS
                                                                                                REPORTED BY THE SYSTEM SUPPLIER
                                                                                                FOR OPERATIONS DURING THE PERIOD.

                                                                96                               PEDCO ENVIRONMENTAL

-------
SCHOLZ IB AND 2B - CHIYODA (CONTINUED)           COMMENTS (CONTINUED)



                                       PROBLEMS INCLUDED A MALFUNCTION




                                       GRID VANE.  AM OPERATOR CAUSED




                                       THE OTHER OUTAGE.
       97                                PEOCO  ENVIRONMENTAL

-------
                  TABLE 3
PERFORMANCE DESCRIPTION FOR OPERATIONAL. FGD SYSTEMS  12/76
IDENTIFICATION NO.
UTILITY NAME
UNIT NAME
UNIT LOCATION
UNIT RATING
FUEL CHARACTERISTICS  COAL   0.6- 3.0 PERCENT SULFUR
                        40

                       KANSAS CITY POWER ft LIGHT

                       HAWTHORN NO 3

                       KANSAS CITY MISSOURI

                            nw
 FGD VENDOR

 PROCESS

 NEW OR RETROFIT

 START UP DATE

 FGD STATUS

 EFFICIENCY,
  PARTICULATES
                      COMBUSTION ENGINEERING

                      LIMESTONE INJECTION 2UET SCRUB

                      RETROFIT

                      11/72

                      OPERATIONAL


                      99 PERCENT
  S02
                      70 PERCENT
 WATER MAKE UP
                      OPEN LOOP 6.0 GPM/MW
 SLUUGE  DISPOSAL
                       UNSTABILIZED SLUUGE DISPOSED  IN UNLINED POND
 UNIT  COST
                      S19/KW  CAPITAL*2.5 MILS/KWH  OP
 OPERATIONAL
  EXPERIENCE
                       KEFER  TO  THE  BACKGROUND  INFORMATION  SECTION  IN  TABLE 3 OF THIS REPORT.
                       THIS INJECTION  ANU  TAIL-END  WtT  SCRUBBING SYSTEM  WAS DESIGNED AN£>  IN-
                       STALLED BY  COMBUSTION  ENGINEERING  AND  PLACED IN SERVICE  NOVEMBER 1972.
                       OPERATION OF  THIS SCRUBBING  SYSTEM DURING 1976  HAS  BEEN  INTERMITTENT.
                       A NUfiUL'R  OF MAJOR MODIFICATIONS  ARE  BEING PERFORMED TO THE SYSTEM  SY THE
                       UTILITY.MAJOR CHANGES  HAVE INCLUDED*CONVERSIOM  FROM A LIMESTONE TO A LIME
                       INJECTION SYSTEM. OEMISTER WASH  SYSTEM MODIFICATIONS. SCRUBBER BED SPRAY
                       SYSTEM MODIFICATIONS.  AND MODIFICATIONS TO THE  GAS  DAMPER ARRANGEMENT.
                                                             98
                                                                                               PEOCO ENVIRONMENTAL

-------
                                                               BACKGROUND INFORMATION
                                                                          ON
                                                        THE HAWTHORN POWER STATION*  UNIT NO. 3
     THE HAWTHORN POWER STATION is LOCATED ON THE NORTH BANK OF THE MISSOURI RIVER IN EAST KANSAS CITY, MISSOURI.  THE PLANT HAS
FIVE ELECTRIC GENERATING UNITS WITH A TOTAL RATED CAPACITY OF 980 MW.  ONLY UNITS 3 AND H ARE RETROFITTED WITH FGD SySTEMS.
     BOILER 3 IS A DRY-BOTTOM PULVERIZED-COAL-FIKED UNIT, MANUFACTURED BY COMBUSTION ENGINEERING AND INSTALLED IN EARLY 1950.
THE PLANT BURNS TWO GRADES OF COAL*  THE COAL WITH HIGHER ASH CONTENT TYPICALLY CONTAINS it PERCENT ASH AND z PERCENT SULFUR.
WITH A HEAT CONTENT OF 11,400 bTU/LB* THE LOWER ASH COAL HAS 11 PERCENT ASH, 0.6 PERCENT SULFUR, AND A HEAT CONTENT OF 9600
BUT/LB.
     THE FGD SYSTEM OPERATES ON LIMESTONE FURNACE INJECTION FOLLOWED BY A FLUE GAS WET-SCRUBBING SYSTEM IN WHICH BOTH THE SULFUR
DIOXIDE AND THE FURNACE-CALCINED LIMESTONE ARE SCRUBBED  AND ALLOWED TO REACT IN A REACTION TANK.
     THE FGD SYSTEM CONSISTS OF TWO IDENTICAL MODULES, EACH CAPABLE OF TREATING 500.000 ACFM OF FLUE GAS AT 300 F.  BYPASSING OF
THE MODULES IS POSSIBLE THROUGH A SYSTEM OF DUCTWORK AND DAMPERS AROUND EACH MODULE,  EACH MODULE CONSISTS OF A GLASS MARBLE BED,
A CHEVRON-TYPE FIBERGLASS DEMISTER, AND A FINNED TUBE REHEATER.  THE DEMISTER WASH SYSTEM USES A SET OF EIGHT WATER LANCES THAT
TURN ON AUTOMATICALLY  TO WASH MUD FROM THE DEMISTERS WHENEVER THE DAMPERS CLOSE.
     THE SPENT LIMESTONE SLURRY FROM THE MODULES IS DISCHARGED INTO A CLARIFIER TANK, AND THE UNDERFLOW IS PUMPED, UNSTABILIZEO,
TO A 160-ACRE UNLlNED  POND, WHICH IS ALSO USED FOR DISPOSAL OF FLY ASH FROM THE OTHER BOILERS.  A PROCESS FLOW DIAGRAM OF THE
LIMESTONE  INJECTIOfc AND TAIL-END WET LIME SCRUBBING SYSTEM INSTALLED ON THIS UNIT IS PRESENTED IN FIGURE 9 OF APPENDIX C.
PROBLEMS AND SOLUTIONS
     THE MAJOR PROBLEMS ENCOUNTERED WITH THE TWO FGD SYSTEMS ON UNITS 3 AND 
-------
                                                               HAWTHORN NO.  3

OPERATING HOURS                                        F&O OPERABILITY IS)
MONTH      BOILER        MODULE 3A      MODULE 3B    MODULE A      MODULE B                     COMMENTS

JUL. 75      56
-------
                                                         HAWTHORN NO. 3 (CONTINUED)

OPERATING HOURS                                        FGD OPERABILITY (X)
MONTH      BOILER        MODULE 3A      MODULE 38    MODULE A      MODULE B                    COMMENTS

MAR. 76        0             0               00              0        RECONVERSION OF MODULE SB'S SPRAY SYSTEM ARRANGE-

                                                                                MENT HAS BEEN COMPLETED.

APR. 76        0             0               00              0        ALSOt THE BYPASS SYSTEM HAS BEEN MODIFIED AND

                                                                                CHANGED TO A SLIDE-GATE DAMPER ARRANGEMENT.

MAY  76        0             0               0          0              0        THE SYSTEM WAS SHUT DOWN DURING THE MONTH DUE TO

                                                                                THE CONTINUATION OF MANPOWER SHORTAGE PROBLEMS.

                                                                                THE UTILITY DID PERFORM SOME CLEANING AND REPAIRS

                                                                                DURING THE MONTH.

JUN. 76      505             196           220         39             
-------
                                                         HAWTHORN NO. 3 (CONTINUED)
OPERATING HOURS                                        FGO OPERABILITY (X)
MONTH      BOILER        MODULE 3A      MODULE HA
                                                                                GO A SERIES OF TESTS TO INSURE COMPLIANCE WITH
                                                                                CITY AND FEDERAL REGULATIONS.
                                                               102                                 PEOCO ENVIRONMENTAL

-------
                  TABLE 3
PERFORMANCE DESCRIPTION FOR OPERATIONAL F60 SYSTEMS  12/76
 IDENTIFICATION NO.

 UTILITY NAME

 UNIT NAME

 UNIT LOCATION

 UNIT RATING

 FUEL CHARACTERISTICS

 F60 VENDOR

 PROCESS

 NEW OK RETROFIT

 START UP DATE

 FGO STATUS

 EFFICIENCY,
  PARTICULATES
  11

 KANSAS CITY POWER £ LIGHT

 HAWTHORN NO H

 KANSAS CITY MISSOURI

  100 MW

 COAL   0.6- 3.0 PERCENT SULFUR

 COMBUSTION ENGINEERING

 LIMESTONE INJECTION *WET SCRUB

 RETROFIT

  6/72

 OPERATIONAL


 99 PERCENT
  S02
 70 PERCENT
 WATEK MAKE UP
 SLUUGE DISPOSAL
 OPEN LOOP 8.0 GPM/MW
 UNSTABILIZED SLUUGE DISPOSED IN UNLINEO POND
 UNIT COST
 OPERATIONAL
  EXPERIENCE
S19/KW CAPITAL*2.2 MILS/KUH OP
 REFER TO THE BACKGROUND INFORMATION SECTION IN TABLE 3 OF THIS REPORT.
 THIS INJECTION AND TAIL-END WET SCRUBBING SYSTEM WAS DESIGNED AND IN-
 STALLED BY COMBUSTION ENGINEERING AND PLACED IN SERVICE AUGUST 1972.
 FGD SYSTEM OPERATIONS DURING 1976 HAVE PROCEEDED ON AN INTERMITTENT
 BASIS. PROBLEMS ENCOUNTERED HAVE INCLUDED PLUGGING IN THE MARBLE BED
 AND REHEAT TUBE BUNDLES, DRAFT LOSSES THROUGH THE DUCTWORK AND PUMP
 FAILURES. THE UTILITY IS NOW CONVERTING THIS SYSTEM FROM LIMESTONE
 INJECTION TO LIME INJECTION AND TAIL-END WET SCRUBBING.
                                                            103
                                                                         PEOCO ENVIRONMENTAL

-------
                                                              BACKGROUND INFORMATION




                                                                        ON




                                                        THE HAWTHORN POEER STATION* UNIT NO.  
-------
                                                 HAWTHORN NO. 
-------
                                                               HAWTHORN  NO.  H

                  OPERATING HOURS                        FGD OPERABILITY (X)
MONTH          BOILER    MODULE HA      MODULE  US      MODULE A   MODULE B                      COMMENTS

JUL. 75         516          41            12fl              B         25          MARBLE  BED  PLUGGING  AND  STRAINER  PROBLEMS  ON  BOTH

                                                                                MODULES.

AUG. 75                     16^            212                                   LOST  HALF OF  BOILER  DUE  TO  NO.  HB I.D.  FAN OUTAGE.

                                                                                BOTH  FGD MODULES WERE SHUT  DOWN TO ENSURE  AGAINST

                                                                                THE LOSS OF THE ENTIRE UNIT.  NEW CHEMISTRY -

                                                                                ATTEMPTING  TO RUN AT 100* SLOWDOWN AND  NEAR 0

                                                                                PERCENT SOLIDS.  EMPHASIS ON  PARTICULATE CONTROL.

                                                                                MAINTAINING PH AT 5  WITHOUT LIMESTONE INJECTION.

SEP. 75         395         206            210             52         53          SCRUBBER MODULES WERE RETURNED  TO SERVICE  ON

                                                                                SEPT. 21 AFTER REPLACEMENT  OF THE ORIGINAL I.D.

                                                                                FAN ON  MODULE 
-------
                                                               HAWTHORN NO. H (CONTINUED)

                  OPERATING HOURS                        FGD OPERAblLITY (X)
MONTH          BOILER    MODULE HA      MODULE HB      MODULE A   MODULE B                     COMMENTS

MOV. 75         720           0            713             0         99         MODULE HA WAS SHUT DOWN DURING THE REPORT PERIOD

                                                                                BECAUSE OF LOSS OF DRAFT THROUGH THE DUCTWORK

                                                                                FROM THE ECONOMIZER TO THE AIR PREHEATER.  THE

                                                                                REHEATER PLUGGED FREQUENTLY UNTIL THE SYSTEM WAS

                                                                                SHUT DOWN.

DEC. 75         6*0           0            103             0         16         BOILER OUTAGE OF 5 DAYS WAS DUE TO A SCHEDULED

                                                                                OVERHAUL.

JAN. 76           0           0              0             00         THE SYSTEM WAS DOWN ALL MONTH BECAUSE OF FROZEN

                                                                                EQUIPMENT AND LINES* MANPOWER WAS ASSIGNED TO A

                                                                                BOILER AND TURBINE OVERHAUL ON ANOTHER UNIT.

FEB. 76         579           0            450             0         76         MODULE HA WAS SHUT DOWN THE ENTIRE MONTH BECAUSE

                                                                                OF CONTINUING LOSS OF DRAFT THROUGH THE DUCTWORK

                                                                                FROM THE ECONOMIZER TO THE AIR PREHEATER.  MARBLE

                                                                                BED PLUGGING AND LOSS OF A RECYCLE PUMP OCCURRED

                                                                                ON MODULE HB,

MAR. 76         706           0             2H             0          3.H       DURING THE REPORT PERIOD THE UNIT'S BYPASS SEALS

APR. 76         550         231            220            H2         HO         WERE REPLACED WITH SLIDE-GATE DAMPERS.

MAY  76         365           99             99            27         27         THE UTILITY REPORTS THE B-SIDE REHEATER IS STILL

JUN. 76         H60         29H             23            65          5         EXPERIENCING PLUGGING PROBLEMS.  ONE SECTION OF

                                                                                THE REHEAT TUBE BUNDLES HAS BEEN REMOVED IN

                                                                                ORDER TO FACILITATE CLEANING AND MAINTENANCE.

JUL. 76                                                                         CURRENTLY? THE UTILITY IS IN THE PROCESS OF

AUG. 76                                                                         MODIFYING THE SCRUBBING SYSTEM FROM A LIMESTONE

                                                                                INJECTION AND TAIL END BASED SYSTEM TO A LIME
                                                               107                                PEOCO ENVIRONMENTAL

-------
                                                               HAWTHORN NO. 
-------
                  TABLE 3
PERFORMANCE DESCRIPTION FOR OPERATIONAL FGD SYSTEMS  12/76
 IDENTIFICATION NO,

 UTILITY NAME

 UNIT NAME

 UNIT LOCATION

 UNIT RATING

 FUEL CHARACTERISTICS

 FGD VENDOR

 PROCESS

 NEW OR RETROFIT

 START UP DATE

 FGD STATUS

 EFFICIENCY,
  PARTICULATES
  42

 KANSAS CITY POWER &  LIGHT

 LA CYGNE  NO 1

 LA CYGNE  KANSAS

  820  MW

 COAL  5,0  PERCENT  SULFUR

 BABCOCK 2 UILCOX

 LIMESTONE SCRUBBING

 NEW

  2/73

 OPERATIONAL


 98 PERCENT
  S02
 76 PERCENT
 WATER MAKE UP
 SLUDGE DISPOSAL
 OPEN LOOP 1.4 GPM/MW
 UNSTABILIZED SLUDGE DISPOSED IN UNLINED POND
 UNIT COST
 OPERATIONAL
  EXPERIENCE
S52/KW CAPITAL * 0.94 MILLS/  KWH OPERATING COSTS
 REFER TO THE BACKGROUND INFORMATION SECTION IN TABLE 3 OF  THIS REPORT,
 THIS 7-MODULE FGD SYSTEM HAS BEEN IN OPERATION SINCE FEBRUARY 1973,
 THE ANNUAL SYSTEM OPERABILITY INDEX VALUE AVERAGED IN EXCESS OF
 76 PERCENT FOR 1974. ANNUAL AVERAGE AVAILABILITY INDEX VALUES FOR
 1975 AND 1976 EXCEEDED 8
-------
                                                           BACKGROUND INFORMATION



                                                                     ON



                                                             LA CYGNE UNIT NO. 1



     THE LA CYGNE: POWER STATION OF KANSAS CITY POWER AND LIGHT COMPANY BEGAN COMMERCIAL OPERATION ON JUNE i, 1973, AS A JOINT



PROJECT OF KANSAS GAS AND ELECTREC COMPANY AND KANSAS CITY POWER & LIGHT COMPANY.  THE STATION IS LOCATED ABOUT 55 MILES SOUTH OF



KANSAS CITY, IN LINN COUNTY, KANSAS.



     ELECTRIC POWER GENERATING FACILITIES CONSIST OF ONE 620 MW COAL-FIRED BASE-LOAD BOILER WITH ASSOCIATED STEAM TURBINES AND



ELECTRIC GENERATORS.  THE PLANT HAS THREE OIL-FIRED BOILERS, USED PRIMARILY FOR STARTUP OF THE LARGE UNIT.  THEIR COMBINED



CAPACITY IS EQUIVALENT TO 28 MW.



     THE BOILER AT LA CYGNE, DESIGNED BY BABCOCK AND WlLCOX, IS A DRY-BOTTOM, PULVERIZED-COAL-FIRED CYCLONE UNIT.  THE COAL



BURNED IS LOW-GRADE. SUBBlTUMlNOUS, WITH AN AS-FIRED HEATING VALUE OF 9000 TO 9700 BTU/L8 AND ASH AND SULFUR CONTENTS OF 25



PERCENT AND 5 PERCENT, RESPECTIVELY.  POLLUTION CONTROL EQUIPMENT ON THIS BOILER CONSISTS OF SEVEN SCRUBBING MODULES, FOR THE



CONTROL OF PARTICULATE AND SULFUR DIOXIDE EMISSIONS.  THIS SCRUBBING SYSTEM WAS DESIGNED AND CONSTRUCTED BY BABCOCK AND WILCOX AS



AN  INTEGRAL PART OF THE POWER GENERATING FACILITIES.  BYPASSING OF THE BOILER'S FLUE GAS AROUND THE FGD SYSTEM IS NOT POSSIBLE.



A PROCESS FLOW DIAGRAM OF THE LA CYGNE AIR QUALITY CONTROL SYSTEM AND RELATED MAJOR EQUIPMENT IS PRESENTED IN FIGURE 10.



PROBLEMS AND SOLUTIONS



     THE FGD INSTALLATION HAS BEEN PLAGUED WITH NUMEROUS PROBLEMS SINCE THE FIRST TRIAL OPERATION ON DECEMBER 26, 1972.  SOME OF



THESE  PROBLEMS,  SUCH  AS VIBRATIONS OF THE INDUCED-DRAFT FANS AND THEIR SENSITIVITY TO IMBALANCE, OCCURRED EVEN BEFORE THE BOILER



WAS FIREC.  AS THESE  FABRICATION PROBLEMS WERE CORRECTED AND THE FGD SYSTEM WENT INTO OPERATION, TWO OTHER TYPES OF PROBLEMS



APPEARED.   THE FIRST  TYPE,  ASSOCIATED WITH THE WET LIMESTONE PROCESS, INCLUDED PLUGGING OF THE DEMISTER AND STRAINERS, WEARING OF



SPRAY  NOZZLES, AND  CORROSION OF REHEATER  TUBES.  PROBLEMS OF THE SECOND TYPE MAY BE UNIQUE TO THE LA CYGNE INSTALLATION IN THAT



THEY CONCERN THE EFFECT OF  THE SCRUBBED FLY ASH ON VISCOSITY AND FLOW CHARACTERISTICS OF THE RECIRCULATED SLURRY, WHICH RESTRICTED



THE MOBILITY OF THE BALLS IN THE ORIGINAL TCA TOWER.  THE FLY ASH CONTENT OF THE FUUE GAS (DUE TO LACK OF PRIMARY PARTICULATE



CONTROLS) IS LARGELY RESPONSIBLE FOR BOTH TYPES OF PROBLEMS.  SEVERAL MODIFICATIONS HAVE BEEN MADE*  THE ORIGINAL TURBULENT



CONTACT ABSORBER'S FLOATING BED WAS REPLACED WITH SIEVE TRAYS NEXT, IN ORDER ALSO TO REDUCE THE EROSIVE EFFECT OF FLY ASH AND



LARGE-SCALE PARTICLES AND TO EXTEND THE LIFE OF THE LIMESTONE SLURRY SPRAY NOZZLES ON THE VENTURI SCRUBBERS, A HYOROCLONE WAS



INSTALLED IN THE SLURRY RECIRCULATION LINE OF EACH MODULE TO CENTRIFUGALLY SEPARATE AND REMOVE THESE PARTICLES FROM THE SYSTEM.



     THE CORROSION ASSOCIATED WITH CONDENSATION OF ACID VAPORS FROM THE GAS ON THE REHEATER TUBE BUNDLES WAS CONTROLLED BY






                                                               110                                PEDCO ENVIRONMENTAL

-------
                                       LA CYGNE NO. 1 (CONTINUED)



INJECTION OF SLIP STREAMS OF HOT AIR FROM THE BOILER'S COMBUSTION AIR HEATER INTO THE SCRUBBED FLUE GASES AT THE INLET TO THE



REHEATER UNITS.  THIS PRACTICE HAS REDUCED THE MAXIMUM GENERATING CAPACITY OF THE BOILER BY LIMITING THE AIR AVAILABLE FOR COAL




COMBUSTION.



     BECAUSE THE FGD SYSTEM INCLUDES NO SPARE MODULES AND IT CANNOT BE BYPASSED. OUTPUT OF THE BOILER is TOTALLY CONTROLLED BY




PERFORMANCE AND AVAILABILITY OF THE FGD MODULES.  PRESENT PROCEDURES CALL FOR CLEANING ONE MODULE EACH NIGHT ON A ROTATIONAL



SCHEDULE AND KEEPING ALL MODULES AVAILABLE DURING THE DAYTIME PEAK PERIODS.  CLEANOUTS REQUIRE THREE MEN FOR A PERIOD OF 10 TO 12



HOURS.  RECENT MODIFICATIONS BY THE UTILITY ON THE SCRUBBER INSTALLATION HAVE RESULTED IN PLANS FOR PROLONGED OPERATIONAL PERIODS,



WITH MODULES STAYING ON-LINE CONTINUOUSLY FOR PERIODS UP TO 3 WEEKS.  THIS PREVENTATIVE MAINTENANCE AND CLEANOUT SCHEDULE HAS* TO



DATE. NOT YET BEEN ADOPTED.



     THE UTILITY IS CURRENTLY PLANNING ADDITIONAL SYSTEM MODIFICATIONS. INCLUDING THE INSTALLATION OF AN EIGHTH SCRUBBING MODULE



SCHEDULED TO BE  IN SERVICE THE SUMP.ER OF 1977.  THE ADDITIONAL MODULE IS ESTIMATED TO COST APPROXIMATELY $5.2 MILLION AND WILL



ENABLE THE  PLANT To INCREASE  ITS MAXIMUM CONTINOUS GENERATING CAPACITY FROM  THE CURRENT 700 MM LEVEL TO 800 MW.  THE ORIGINAL



AIR QUALITY CONTROL SYSTEM DESIGN  ALLOTTED  ADDITIONAL SPACE FOR  JUST SUCH A  SYSTEM EXPANSION.  OTHER SYSTEM MODIFICATIONS INCLUDE*



CHANGING THE I.D. FANS  IN ORDER TO MINIMIZE OR  ELIMINATE A FAN PARALLELING PROBLEM* CONTINUATION OF EXPERIMENTS AND MINOR CHANGES



IN ORDER TO IMPROVE SYSTEM MECHANICAL EFFICIENCY AND DECREASE OPERATING EXPENSES.
                                                               Ill                                PEDCO ENVIRONMENTAL

-------
                               FGO SYSTEM AVAILABILITY



                            LA CYGNE UNIT NO. 1
PERCENT AVAILABLITY-BY MODULE
MONTH BOILER HOURS
JAN.
FEB.
MAR.
APR.
MAY
JUN.
JUL.
AUG.
SEP.
OCT.
NOV.
DEC.
JAN.
FEB.
MAR.
APR.
MAY.
JUN.
JUL.
AUG.
74
74
74
74
74
74
74
74
74
7
-------
                                                     FGD SYSTEM AVAILABILITY (CONTINUED)

                                                             LA CYGNE UMT NO. 1

                                 PERCENT AVAILABLITY-BY MODULE
MONTH     BOILER HOURS     A     B     C     0     E     F     G         AVERAGE                    COMMENTS

SEP. 75       610         78    64     84    65     79     76    74        80        SYSTEM SHUTDOWN OCT. 16, 1975 OWING TO

                                                                                     PROBLEMS WITH GENERATOR AND 1.0. AIR FAN.

                                                                                     SYSTEM REMAINED INOPERATIVE THROUGHOUT THE

                                                                                     MONTH.

OCT. 75       231         66    77     46    74     72     73    65        68        AVAILABILITY FIGURES FOR OCTOBER AND

NOV. 75       346         93    90     80    93     96     89    94        91        NOVEMBER 00 NOT INCLUDE THE OUTAGE TIME FROM

DEC. 75       597         91    67     81    65     87     69    84        86        OCTOBER 16 TO NOVEMBER 13.  BOILER OUTAGES

                                                                                     OF 80, 50, AND U HOURS, TOTALING 141 HOURS,

                                                                                     OCCURRED DURING DECEMBER.

JAN. 76       616         66    85     91    72     84     52    64        63

FEB. 76       594         94    90     66    91     92     93    95        92

MAR. 76       643         92    90     88    93     94     91    91        91

APR. 76                                      BOILER OVERHAUL                         THE SYSTEM WAS SHUT DOWN ON APRIL 6 FOR A

                                                                                     SCHEDULED BOILER AIR PREHEATER AND STACK

                                                                                     BREECHING OVERHAUL.  DURING THIS OUTAGE SOME

                                                                                     MAINTENANCE WAS PERFORMED ON THE SCRUBBER

                                                                                     DUCTWORK, PRIMARILY BECAUSE OF CORROSION

                                                                                     PROBLEMS.

MAY  76       436         96    92     93    96     69     95    96        94        THE SCHEDULED UNIT OUTAGE ENDED MAY 10 WHEN

                                                                                     THE SYSTEM WAS RESTARTED.  DURING THE

                                                                                     REMAINDER OF THE MONTH FOUR UNIT OUTAGES

                                                                                     WERE ENCOUNTERED, TOTALING OVER 70 HOURS.
                                                               113                                PEDCO ENVIRONMENTAL

-------
                                                     FGD SYSTEM AVAILABILITY  (CONTINUED)
                                                             LA CYGNE UNIT  NO.  1
MONTH     BOILER HOURS     A
JUN. 76                   99
JUL. 76                   96
 PERCENT AVAILABLITY-BY MODULE
 B     C     D     E     F     6
                                95
             95
             93
             93
             93
                                                           93
      91
        AVERAGE
          93
AUG. 76
93
92
                                                    92
90
88
92
SEP. 76
OCT. 76
        TURBINE REPAIR
        TURBINE REPAIR
               COMMENTS
FOUR FORCED MINOR SCRUBBER OUTAGES OCCURED
DURING THE MONTH, RESULTING IN A TOTAL
AVERAGE SYSTEM AVAILABILITY OF 93.33 PERCENT.
THE UNIT RECORDED ITS LARGEST MU-HOUR MONTH
SINCE INITIATION OF COMMERCIAL OPERATION.
TWO MINOR SCRUBBER OUTAGES OCCURRED DURING
THE MONTH.
THE SYSTEM WAS TAKEN OUT OF SERVICE AUGUST
2<» FOR REPAIR OF A TURBINE BLADE.  THE
UTILITY TOOK ADVANATAGE OF THIS OUTAGE
PERIOD TO PROCEED WITH COATING THE STACK
INNER STRUCTURE WITH PLASTITE H005.  THE
AUGUST AVAILABILITY FIGURES DO NOT INCLUDE
THIS OUTAGE TIME.
UNIT NO. 1 REMAINED OUT OF SERVICE ALL OF
SEPTEMBER AND THE FIRST THREE WEEKS OF
OCTOBER BECAUSE OF COMPLETION TO TURBINE
BLADE REPAIRS WHICH COMMENCED ON AUGUST 2H.
THE SYSTEM WAS RETURNED TO SERVICE ON
OCTOBER 20.  OPERATION WAS INTERMITTENT
PENDING TURBINE BLADE REBALANCING AND RE-
ESTABLISHMENT OF NORMAL OPERATING CONDITIONS.
                                                               11*
                                                                  PEOCO ENVIRONMENTAL

-------
          F60 SYSTEM AVAILABILITY (CONTINUED)



                            LA CYGNE UNIT NO. 1



PERCENT AVAILABILITY - BY MODULE
MONTH
NOV. 76
DEC. 76
BOILER HOURS
627
706
A
95
87
B
93
89
C
94
81
D
95
94
E
94
94
F
93
95
e
94
91
AVERAGE
94
90
                                                                  COMMENTS



                                                    DURING THE MONTH OF DECEMBER THE UTILITY



                                                    CONDUCTED SOME MINOR REPAIR AND MODIFICATION




                                                    WORK ON THE AGCS, SPECIFICALLY A-MODULE



                                                    EXPERIENCED SOME VENTURI RECYCLE PUMP



                                                    PROBLEMS AND THE C-MODULE'S REHEAT STEAM




                                                    TUBE BUNDLES WERE INCREASED IN NUMBER FROM
                              115
PEDCO ENVIRONMENTAL

-------
                  TABLE 3
PERFORMANCE DESCRIPTION FOR OPERATIONAL FGO SYSTEMS  12/76
 IDENTIFICATION NO.


 UTILITY NAME


 UNIT NAME


 UNIT LOCATION


 UNIT RATING


 FUEL CHARACTERISTICS


 FGD VENDOR


 PROCESS


 NEW OR RETROFIT


 START UP DATE


 FGD STATUS


 EFFICIENCY,
  PARTICULATES
 HS


KANSAS POWER & LIGHT


LAWRENCE NO «f


LAWRENCE KANSAS


 125 MW


COAL 0.5 PERCENT SULFUR


COMBUSTION ENGINEERING


LIMESTONE INJECTION SUET SCRUB


RETROFIT


12/66


OPERATIONAL



99 PERCENT
  S02
75 PERCENT
 WATER MAKE UP
 SLUUGE DISPOSAL
OPEN LOOP
              GPM/MW
UNSTABILIZED SLUDGE DISPOSED IN UNLINED POND
 UNIT COST
 OPERATIONAL
  EXPERIENCE
REFER TO BACKGROUND INFORMATION SECTION IN TABLE 5 OF THIS REPORT.
THE ORIGINAL FliD SYSTEM FOR THIS UNIT WAS PLACED IN SERVICE DECEMBER
1568.  IN ACHIEVING AN OPTIMUM MODE OF OPERATION, THE PHYSICAL SCRUBBER
PLANT WAS CONSUMED* REQUIRING REPLACEMENT WITH A NEW VENTUHI ROD
SCRUBBER AND SPRAY TOWER ABSORBER SYSTEM SUPPLIED BY COMBUSTION
ENGINEERING.INSTALLATION OF THE NEW SYSTEM IS COMPLETE.INITIAL OPERATION
SHOULD COMMENCE IN THE EARLY PART OF 1977* THE UNIT WAS DOWN THROUGH-
OUT THE REPORT PERIOD BECAUSE OF A SCHEDULED TURBINE OVERHAUL.
                                                            116
                                                                        PEDCO ENVIRONMENTAL

-------
                                                           BACKGROUND INFORMATION
                                                                     ON
                                                   THE LAWRENCE POWER STATION*  UNIT NO. H
     LAWRENCE POWER STATION'S UNIT NO. H IS A CYCLIC LOAD STEAM BOILER EQUIPPED TO BURN COAL, NATURAL GAS SUPPLEMENTED WITH OIL,
OR COMBINATIONS OF THESE THREE FUELS.  THE BOILER WAS BUILT BY COMBUSTION ENGINEERING AND PLACED IN SERVICE IN 1959.  GENERATING
CAPACITY VARIES FROM 125 MW TO 143 MW WITH THE TYPE OF FUEL BEING BURNED.  RETROFITTING WITH AN FGD SYSTEM IN NOVEMBER 1968
INTRODUCED ADDITIONAL PRESSURE DROP IN THE FLUE GAS SYSTEM AND REDUCED BOILER CAPACITY TO 115 MW.
     THE COAL NOW BURr4£D AT THE. LAWRENCE POWER PLANT IS A LOW-SULFUR SOUTHEAST WYOMING COAL, HAVING AN AVERAGE HEATING VALUE OF
10,000 BTU/LB AND SULFUR AND ASH CONTENTS OF 0.5 AND 11 PERCENT RESPECTIVELY.
     THE ORIGINAL SCRUBBING SYSTEM INCLUDED TWO MODULES, EACH SIZED TO HANDLE 150,000 SCFM OF FLUE GAS. EACH MODULE CONTAINS A
SINGLE-STAGE MARBLE BED SCRUBBER FOLLOWED BY A CHEVRON DEMISTER AND INDIRECT STEAM REHEATER. ORIGINALLY* BOTH MODULES WERE
FITTED WITH BYPASS DUCTS AND HYDRAULIC SEAL DAMPERS,  WHICH WERE LATER REMOVED BECAUSE OF EXTENSIVE CORROSION AND PLUGGING.
     THE PLANT HAS FACILITIES FOR STORING AND HILLING THE LIMESTONE, WHICH CONTAINS 93 PERCENT CALCIUM CARBONATE, 6 PERCENT
SILICA, AND 1 PERCENT MAGNESIUM CARBONATE.
     SPENT SLURRY DISCHARGED FROM THE ORIGINAL SYSTEMS FITTED ON UNITS 4 AND 5 WERE SENT TO  THREE INTERCONNECTED UNLINEO DISPOSAL
PONDS WITH CAPACITIES OF 16, 26, AND  4 ACRES, RESPECTIVELY. KANSAS RIVER WATER (MAKE-UP) WAS ADDED TO THE LATTER POND. THE
SUPERNATANT FROM THIS POND WAS RECYCLED. THE UNSTABILIZEO SLUDGE SOLIDIFIED AND SET-UP IN THE DISCHARGE PONDS.
PROBLEMS AND SOLUTIONS
     PROBLEMS WITH THE  FGD SYSTEM ON  BOILER NO. 4 HAVE INCLUDED BUILDUP AND PLUGGING OF THE  INLET DUCT WHERE HOT GASES ENTER THE
SCRUBBERS, EROSION OF SCRUBBERS WALLS, CORROSION OF SCRUBBERS INTERNALS, BUILDUP ON ID FAN ROTORS, AND PLUGGING OF DRAIN LINES,
MARBLE BEOS, AND DEMISTERS.  LOW S02  REMOVAL WAS CAUSED BY OVERBURNING OF THE LIMESTONE AND  DROPOUT OF THE LIME WITH THE ASH IN
THE BOTTOM OF THE SCRUBBER.
     THE SCRUBBERS WERE MODIFIED  IN  1969 BY RAISING THE DEMISTER  AND ADDING SOOT BLOWERS IN THE INLET DUCT AND REHEATER TO REDUCE
PLUGGING.  NEW SPRAY NOZZLES WERE ALSO INSTALLED.  REHEATER PLUGGING WAS ELIMINATED BY REPLACING COPPER REHEAT COILS WITH A
CARBON STEEL UNIT HAVING WIDELY SPACED FINS.
     MAJOR MODIFICATIONS IN 1970 WERE SANDBLASTING AND COATING OF THE INTERIOR OF THE SCRUBBERS, REPLACEMENT OF ALL INTERNAL
STEEL PIPES WITH PLASTIC AND FIBERGLASS, AND REPLACEMENT OF STAINLESS STEEL DEMISTERS WITH FIBERGLASS.  SINCE DEMISTER PLUGGING
WAS NOT COMPLETELY ELIMINATED* THE UNIT WAS WASHED MANUALLY EVERY NIGHT TO MAINTAIN THE REQUIRED OUTPUT.
                                                               117                                PEDCO ENVIRONMENTAL

-------
LAWRENCE UNIT NO.  <* (CONTINUED)



     THE MODIFICATIONS IN THE SUMMER OF 1972 ON THE TWO FGD MODULES INCLUDED ENLARGEMENT OF THE CRYSTALLIZATION TANK. AND



INSTALLATION OF NEW PLASTIC SPRAY NOZZLES,  NEW SLURRY PUMPS ANU STRAINERS?  AND NEW MULTIPLE MIXERS IN THE TANK.



     PROBLEMS THAT REMAINED INCLUDED CORROSION, INEFFICIENT DAMPERS, EXPANSION JOINT FAILURE, DEMISTER FOULING, RAPID EROSION



OF THE SLURRY PUMP, AND VALVE FAILURE.   OPERATION OF THE FGD SYSTEM SINCE THE FALL OF 1973 HAS BEEN THE MOST SUCCESSFUL TO DATE.



     OPERATION OF  THE SCRUBBER SYSTEM ON THE WYOMING COAL HAS PROVED TO BE MORE EFFICIENT AND ECONOMICAL THAN EARLIER OPERATIONS



BECAUSE A LESSER DEGREE OF S02 REMOVAL IS KEOUIREO FOR COMPLIANCE.   THE SCRUBBER SYSTEM IS STILL OPERATING IN THE HIGH-SOLIDS



MODE AS AN S02 AND PARTICULATE REMOVAL SYSTEM. NORMAL MANUAL CLEANING REQUIREMENTS HAVE BEEN REDUCED TO TWO H-HOUR SHIFTS PER




SCRUBBER PER WEEK.



     IN 197
-------
                                                               LAURENCE NO. 4
MONTH
JUL. 75
AUG. 75


SEP. 75
OCT. 75
NOV. 75
DEC. 75
JAN. 76
FEB. 76
MAR.  76
APR.  76
MAY 76
JUN.  76
JUL.  76
AUG.  76
BOILER
   OPERATING HOURS
MODULE A   MODULE B
  AVAILABILITY
MODULE A   MODULE B
               NOT LOGGED
               NOT LOGGED
                NOT  LOGGED
                NOT  LOGGED
                         COMMENTS
THE FGD SYSTEM HAS OPERATED SATISFACTORILY FOR OVER A YEAR.
AVAILABILITY IS REPORTED TO BE ADEQUATE FOR THE OPERATION
OF THIS STATION.  STATION LOAD IS REDUCED TO 50 PERCENT>
EVEKY NIGHT.  THEREFORE, ONE OF THE MODULES CAN BE TAKEN
OFF-LINE NIGHTLY FOR CLEANING OR REPAIR.  WYOMING COAL (>0.5
 PERCENT SULFUR) IS BEING BURNED IN THE BOILER. SOME
 NATURAL GAS HAS BEEN BURNED SINCE JUNE 20.
BURNED COAL 100 PERCENT OF TIME.  EACH MODULE SHUT DOWN
 ONCE PER WEEK FOR INSPECTION AND CLEAN-UP. NO BOILER
 OUTAGES OCCURRED DURING THE JULY-AUGUST PERIOD.
                                                PRESENT PROJECTIONS BY THE UTILITY CALL FOR THIS UNIT TO BE
                                                AVAILABLE 330 DAYS DURING 1976.  THE FUEL CONSUMPTION WILL
                                                BE 80 PERCENT COALt 12 PERCENT NATURAL GAS, AND 6 PERCENT
                                                FUEL OIL.  THE UTILITY IS REPLACING THIS SCRUBBER SYSTEM
                                                WITH A VENTURI-ROD FOLLOWED BY A SPRAY TOWER.
                                                            NO INFORMATION WAS REPORTED BY THE UTILITY FOR THE PERIOD.
                                                            NO INFORMATION WAS REPORTED BY THE UTILITY FOR THE PERIOD.
                                                               119
                                                                                        PEDCO ENVIRONMENTAL

-------
                                                               LAURENCE  NO.
MONTH     BOILER

SEP. 76

OCT. 76

NOV. 76

DEC. 76
      OPERATING HOURS
   MODULE A   MODULE 8
  AVAILABILITY
MODULE A   MODULE B
TURBINE OVERHAUL AND REPAIR
COMMENTS
                        THE UTILITY REPORTS THAT THE UNIT REMAINED OUT OF SERVICE

                        THROUGHOUT THE REPORT PERIOD AS A SCHEDULED TURBINE

                        OVERHAUL, WHICH COMMENCED IN MID-SEPTEMBER* CONTINUED. THE

                        NEW EMISSION CONTROL SYSTEM, CONSISTING OF AN ESP FOLLOWED

                        BY A ROD SECTION AND SPRAY TOWER SCRUBBING SYSTEM, HAS

                        BEEN INSTALLED ON THIS UNIT. INITIAL OPERATION OF THE

                        SYSTEM WILL COMMENCE FOLLOWING COMPLETION OF THE TURBINE

                        OVERHAUL. THE UNIT WILL CONTINUE TO FIRE LOW SULFUR

                        WYOMING COAL (0.5& SULFUR* 10,000 BTU/LB).
                                                               120
                                                                               PEDCO ENVIRONMENTAL

-------
                  TABLE 3
PERFORMANCE DESCRIPTION FOR OPERATIONAL FGD SYSTEMS  12/76
 IDENTIFICATION NO.


 UTILITY NAME


 UNIT NAME


 UNIT LOCATION


 UNIT RATING


 FUEL CHARACTERISTICS


 FGD VENDOR


 PROCLSS


 NEW OR RETROFIT


 START UP DATE


 FGD STATUS


 EFFICIENCY,

  PARTICULATES
KANSAS POWER & LI6HT


LAWRENCE NO 5


LAWRENCE KANSAS


 100 HW


COAL 0.5 PERCENT SULFUR


COMBUSTION ENGINEERING


LIMESTONE INJECTION iWET SCRUB


NEW


11/71


OPERATIONAL



99 PERCENT
  S02
65 PERCENT
 hlATEK MAKE  UP
OPEN LOOP 3.0 GPM/MW
 SLUDGE  DISPOSAL
UNSTABILIZED SLUDGE DISPOSED IN UNLINEO POND
 UNIT COST
  OPERATIONAL
   EXPERIENCE
REFER TO BACKGROUND INFORMATION SECTION IN TABLE 3 OF THIS REPORT.
THE ORIGINAL FttD SYSTEM FOR THIS UNIT WAS PLACED IN SERVICE NOVEMBER 1971
RENTLY BURNING LOW SULFUR WYOMING COAL. THE OPERATION OF THE SCRUBBER HAS
IN ACHIEVING AN OPTIMUM MODE OF OPERATION. THE PHYSICAL SCRUBBER PLANT
WAS CONSUMED! REQUIRING REPLACEMENT WITH TWO NEW VENTURI ROD
SCRUBBERS AND SPRAY TOWER ABSORBERS SUPPLIED BY COMBUSTION ENGINEERING.
IS PROCEEDING ON POURING OF THE FOUNDATION AND ERECTION OF THE
STRUCTURAL STEEL.  THE BOILER IS IN SERVICE. FIRING FUEL OIL.
                                                            121
                                                                        PEOCO ENVIRONMENTAL

-------
                                                           BACKGROUND INFORMATION




                                                                     ON



                                                   THE LAWRENCE POWER STATION*  UNIT NO. 5



     UNIT NO. 5 AT LAWRENCE POWER STATION IS A CYCLIC-LOAD STEAM BOILER EQUIPPED TO BURN COAL. NATURAL GAS SUPPLEMENTED WITH OILt



OR COMBINATIONS OF THESE FUELS.  THE BOILERt PLACED IN SERVICE IN 1971t HAS A RATED CAPACITY OF <»00 MW WHEN BURNING COAL AND



NATURAL GAS.



     THE COAL NOW BURNED AT THE LAURENCE POWER PLANT IS A LOW-SULFUR SOUTHEAST WYOMING COAL, HAVING AN AVERAGE HEATING VALUE OF




10,000 BTU/LB AND SULFUR AND ASH CONTENTS OF 0.5 AND 11 PERCENT RESPECTIVELY.



     THE BOILER'S ORIGINAL FGD SYSTEM WAS SUPPLIED BY COMBUSTION ENGINEERING AND PLACED IN SERVICE IN 1971. ORIGINAL EQUIPMENT



INCLUDED 6 IDENTICAL MODULES WITH A CAPACITY OF 150,000 SCFM/MODULE. EACH MODULE CONSISTS OF A SINGLE-STAGE MARBLE BED SCRUBBER



FOLLOWED BY A CHEVRON-TYPE DEMISTER AND INDIRECT STEAM REHEATER. ALL THE MODULES ARE FITTED WITH BY-PASS DUCTS AND HYDRAULIC



SEAL DAMPERS. THE PLANT INCLUDES FACILITIES FOR STORING AND MILLING LIMESTONE (COMPOSITION* 93 PERCENT CALCIUM CARBONATE* 6



PERCENT SILICA, AND 1 PERCENT MAGNESIUM CARBONATE).



     SPENT SLURRY FROM THE UNIT ALONG WITH THE SLURRY FROM UNIT NO. 
-------
LAWRENCE UNIT NO. 5 (CONTINUED)



     THE UTILITY HAS RE-EVALUATED THE FUTUKE OF SCRUBBING APPLICATION ON THIS POWER-GENERATING UNIT. THE UTILITY IS NOW




FOLLOWING A COURSE SIMILAR TO THAT OF UNIT *, CONVERTING THE MARBLE BED SCRUBBERS To A TWO TRAIN ROD AND SPRAY TOWER SCRUBBING




SYSTEM. AUOITIONAL DATA AND INFORMATION ON THE DEVELOPMENT OF FGU TECHNOLOGY FOR THIS UNIT IS PRESENTED IN THE PERFORMANCE




TABLE BELOW
                                                                123                                PEOCO  ENVIRONMENTAL

-------
MONTHS
  OPERATING HOURS
BOILER     FGO MODULES
JUL. 75

AUG. 75

SEP. 75

OCT. 75

NOV. 75

DEC. 75

JAN. 76
FEB. 76

MAR. 76

APR. 76

MAY 76

JUN. 76

JUL. 76

AUG. 76

SEP. 76

OCT. 76
            NOT LOGGED
            NOT LOGGED
            NOT LOGGED
            NOT LOGGED
            NOT LOGGED
                  LAWRENCE NO. 5


                      COMMENTS

WYOMING COAL IS BEING BURNED IN THIS UNIT.  FGO SYSTEM AVAILABILITY IS REPORTED TO BE

ADEQUATE FOR OPERATION OF THIS STATION.  SINCE STATION LOAD IS REDUCED TO 50 PERCENT

EVERY NIGHT. AS MANY AS FOUR MODULES CAN BE SHUT DOWN FOR CLEANING AND REPAIR EACH

EVENING.

FGD UNITS WERE OFF-LINE MOST OF JUNE FOR MAJOR REBUILDING OF THE SPRAY SYSTEMS IN ALL

MODULES.  SOME OIL WAS BURNED TO ALLOW BYPASSING OF THE REPAIR.

OIL AND GAS WERE BURNED IN JULY AND AUGUST.  NO FGD OPERATION.



GAS AND OIL BURNED ON A PART-TIME BASIS DURING SEPTEMBER AND OCTOBER.  BOILER OUTAGE

WAS DUE TO INSPECTION, TURBINE REPAIR, AND REPLACEMENT OF THE SLURRY TANK SCREEN.
PROJECTIONS BY THE UTILITY FOR THIS UNIT CALL FOR 330 DAYS OF OPERATION IN 1976 WITH

FUEL CONSUMPTION BEING 60 PERCENT COAL, 25 PERCENT FUEL OIL, AND 15 PERCENT NATURAL

GAS.  LIKE UNIT 4, THIS UNIT MAY BE CONVERTED TO A VENTRI-ROD AND SPRAY TOWER

SCRUBBING SYSTEM*



NO  INFORMATION WAS REPORTED BY THE UTILITY FOR THE PERIOD.



NO  INFORMATION WAS REPORTED BY THE UTILITY FOR THE PERIOD.



NO  INFORMATION WAS REPORTED BY THE UTILITY FOR THE PERIOD.



NO  INFORMATION WAS REPORTED BY THE UTILITY FOR THE PERIOD.
                                                                                                  PEOCO ENVIRONMENTAL

-------
LAWRENCE NO.5(CONTINUED)
MONTHS

NOV. 76

DEC. 76
  OPERATING HOURS
BOIL£R     FGD MODULES
                      COMMENTS
THE UTILITY REPORTS  THAT THE INSTALLATION OF THE NEW ROD AND SPRAY TOWER SCRUBBING
SYSTEM IS NOW IN PROGRESS. THE SYSTEM WILL INCLUDE TWO SCRUBBING TRAINS, EACH
HANDLING 50 PERCENT OF THE FLUE GAS CAPACITY. FOUNDATION AND STRUCTURAL STEEL
ERECTION HAS BEEN COMPLETED. SOME OF THE BREECHING HAS BEEN INSTALLED. THE FGO
SYSTEM WILL OPERATE ON A FULLY AUTOMATED BASIS. KP&L REPORTS THAT C-E HAS
ENCOUNTERED SOME PROBLEMS WORKING OUT AND FINE-TUNING SOME OF THE LOGIC CIRCUITS.
THE BOILER HAS BEEN FIRING NO.2 FUEL OIL WHILE THE NEW SCRUBBING SYSTEM IS BEING
INSTALLED. THE SYSTEM WILL TREAT FLUE GAS RESULTING FROM THE BURNING OF LOW SULFUR
(0.5 PERCENT) WYOMING COAL.
                                                               125
                                                                                    PEDCO ENVIRONMENTAL

-------
                  TABLE 3
PERFORMANCE DESCRIPTION FOR OPERATIONAL F60 SYSTEMS  12/76
 IDENTIFICATION NO.

 UTILITY NAME

 UNIT NAME

 UNIT LOCATION

 UNIT HATING

 FUEL CHARACTERISTICS


 FGD VENDOR

 PROCESS

 NEW OK RETROFIT

 START UP OATE

 FGD STATUS

 EFFICIENCY,
  PARTICIPATES
  H7


 KENTUCKY UTILITIES


 GRC-N RIVER   UNITS 1 AND 2


 CENTRAL CITY KENTUCKY


   6
-------
                                                                BACKGROUND INFORMATION
                                                                          ON
                                                               GREEN RIVER POWER STATION
     THE GREEN RIVER POWER STATION IS WHOLLY OWNED AND OPERATED BY THE KENTUCKY UTILITIES COMPANY AND SITUATED ON THE GREEN RIVER,
NEAR CENTRAL CITY IN MUHLENBERG COUNTY, KENTUCKY. THE STATION CONSISTS OF TWO TURBINE GENERATORS AND FOUR COAL-FIRED BOILERS.
     AS THE RESULT OF A CONTRACT AWARDED BY KENTUCKY UTILITIES (KU) TO AMERICAN AIR FILTER (AAF), A TAIL.END WET LIME SCRUBBING
SYSTEM WAS DESIGNED AND INSTALLED ON BOILERS 1, 2, AND 3 AT THE GREEN RIVER POWER STATION.
     THE FLUE GAS oESULFURIZATION (FGD) AND PARTICIPATE REMOVAL SYSTEM CONSISTS OF ONE SCRUBBER MODULE DESIGNED TO HANDLE A
MAXIMUM OF 360,000 ACFM OF FLUE GAS AT 300 F.  THE BLOW-THROUGH SCRUBBER MODULE CONTAINS A VARIABLE-THROAT FLOODED-ELBOW VENTURI
FOR FLY ASH REMOVAL AND A MOBILE BED CONTACTOR FOR SULFUR DIOXIDE REMOVAL.  ENTRAINED WATER DROPLETS ARE REMOVED VIA A CENTRIFUGAL
OEMISTER BEFORE DISCHARGE TO A LOCAL STACK.  THE SLURRY RECYCLE/DISCHARGE SYSTEM CONSISTS OF ONE COMMON ACID RESISTENT TANK WITH
TWO PARTITIONS MAKING A TOTAL OF THREE COMPARTMENTS.  COMPLETION OF CHEMICAL REACTIONS, RECIRCULATION OF SOLUTION AND WASTES
DISCHARGE ARC CONTROLLED AND MONITORED HERE.  MECHANICAL COLLECTORS ARE PROVIDED UPSTREAM OF THE WET SCRUBBING SYSTEM FOR PRIMARY
PARTICULATE MATTER REMOVAL.
     BOILERS 1, 2, AND 3 ARE PULVERIZED COAL-FIRED UNITS SERVICING TWO TURBINES, EACH RATED AT 32 MW (GROSS).  THE FUEL BURNED IN
THESE UNITS IS PRIMARILY A HIGH SULFUR WESTERN KENTUCKY COAL  (10,797 BTU/LB.t 3.6 TO t.O PERCENT SULFUR, 13 TO 1H PERCENT ASH).
THE FGD SYSTEM CAN BE BYPASSES THROUGH A  SERIES  OF DUCTWORK AND GUILLOTINE DAMPERS.
     A TURNKEY CONTRACT FOR THIS PROJECT  WAS AWARDED TO AAF IN JUNE 1973.  CONSTRUCTION AND INSTALLATION OF THE SYSTEM WAS COM-
PLETED BY MID-SEPTEMBER 1975.  FOLLOWING  GENERAL ELECTRICAL AND MECHANICAL DEBUGGING, WHICH INCLUDED OPERATION OF THE AGITATORS
AND PUMPS, THE UNIT  WAS PUT IN SERVICE ON AIR AND WATER ONLY  IN AUGUST 1975.  DURING THIS OPERATION PERIOD, THE FLOW OF GAS AND
LIQUID* OPERATION OF DAMPERS, AND SPRAY PATTERNS WERE MONITORED AND CALIBRATED.  NEXT, THE SYSTEM WAS OPERATED ON AIR AND WATER
UNDER NORMAL PROCESS CONDITIONS.  THE PURPOSE OF THIS PHASE OF OPERATION WAS TO DETECT ANY EARLY FAILURES OF A MECHANICAL NATURE
PRIOR TO THE INITIAL FLUE GAS RUN.
     THE FLUE GAS RUN COMMENCED THE MORNING OF SEPTEMBER 13,  1975.  INITIAL OPERATION PROCEEDED ON A HALF-LOAD BASIS BECAUSE ONE
OF THE TURBINE GENERATORS WAS OUT OF SERVICE FOR OVERHAUL AND REPAIRS.  IN ADDITION, OPERATION OF THE SCRUBBING SYSTEM WAS CON-
DUCTED ON AN OPEN-WATER-LOOP BASIS.  THIS MODE OF OPERATION (HALF LOAD, OPEN LOOP) CONTINUED INTO THE FIRST QUARTER OF 1976.  IN
MARCH, THE SYSTEM BEGAN OPERATION AT FULL LOAD CAPACITY IN A  CLOSED-WATER-LOOP MODE.  GUARANTEED SULFUR DIOXIDE REMOVAL EFFICIENCY
IS 60 PERCENT FOR 3.6 PERCENT SULFUR COAL HAVING A HEATING VALUE EQUAL TO OR GREATER THAN 11*000 BTU/LB.

                                                               127                                PEDCO ENVIRONMENTAL

-------
                                                      GREEN RIVER POWER  STATION (CONTINUED)



ADDITIONAL INFORMATION ON THE OPERATION OF THIS SYSTEM IS PRESENTED IN THE PERFORMANCE TABLE THAT FOLLOWS.  A GENERAL PROGRESS



FLOW DIAGRAM IS PRESENTED IS FIGURE 12 OF APPENDIX C.
                                                               128                                PEDCO ENVIRONMENTAL

-------
            TOTAL
PERIOD  PERIOD 
DEC. 75      7«m
AVAILABILITY = 7HX
RELIABILITY = 76X
OPERABILITY = 65X
UTILIZATION = 35X


JAM. 76      7
-------
                                                          F6D SYSTEM AVAILABILITY  (CONTINUED)

                                                               GREEN RIVEK NOS.  1  AND 2
            TOTAL         BOILER
RIOD  PERIOD HR    OPERATION HR
APR. 76      720

AVAILABILITY = 90%

RELIABILITY = 100*

OPERABILITY = 100%

UTILIZATION = 778

HAY  76      7HH

AVAILABILITY = 61%

RELIABILITY = 100%

OPERABILITY = 100%

UTILIZATION = 61%

JUN. 76      720

AVAILABILITY = 100%

RELIABILITY = 99%

OPERABILITY = 99%

UTILIZATION = 82*

JUL. 76      7nt

AVAILABILITY = 90%

RELIABILITY = 99S

OPERABILITY = 98%

UTILIZATION = 72%

AUG. 76      7HH

AVAILABILITY = 97%
552
        MODULE
AVAILABILITY  HR

        6<»8
  NOt riR. MODULE
   CALLED UPON
TO OPERATE

      552
  HR. MODULE
OPERATE

    552
        COMMENTS
THE UTILITY MADE A PRIOR COMMITMENT
TO RUN AT 100 PWRCENT OPERABILITY
DURING THE MONTH OF APRIL.
H56
        606
                       
-------
            TOTAL
PERIOD  PERIOD (HK)

RELIABILITY = 97*

OPERABILITY = 97*

UTILIZATION = 97S

SEP. 76      720

AVAILABILITY = 86*

RELIABILITY = 100%

OPERABILITY = 100*

UTILIZATION = 79*
OCT. 76

AVAILABILITY =  100JS

RELIABILITY = 1005

OPERABILITY = 100%

UTILIZATION = 9>»S

NOV. 76      720
AVAILABILITY =  100%
OPERABILITY = 100*
RELIABILITY = 98S
UTILIZATION = 98*
OtC. 76       7<»'»
AVAILABILITY =  73*
OPERABIHTY = 97*
RELIABILITY = 67*
UTILIZATION = 70*
                                                          FGD SYSTEM AVAILABILITY  {CONTINUED)

                                                               GREEN RIVEK NOS. 1  AND 2
    BOILER
OPERATION (HR)
     MODULE
AVAILABILITY (HK)
NO. HR. MODULE
 CALLED UPON
 TO OPERATE
HR. MODULE
 OPERATE
      571
     617
    571
   571
      699
                        699
                     699
     701*
     536
     720
     539
    70«t
    591
    704
    517
          COMMENTS
BECAUSE OF VIBRATION IN THE SCRUB-
BER BOOSTER I.D. FAN, NECESSITATING
SYSTEM SHUTDOWN AND REPAIR.
HALF-LOAD OPERATIONS WERE CONDUCTED
THROUGHOUT THE PERIOD BECAUSE OF
BEARING PROBLEMS TO ONE OF THE TWO
TURBINE GENERATING UNITS.  SOME
MINOR FAN PROBLEMS, WHICH DID NOT
REQUIRE ANY FORCED OUTAGE TIME,
WERE ENCOUNTERED DURING THE PERIOD.
DURING THE PERIOD SOME FLUE GAS WAS
BY-PASSED AROUND THE SYSTEM WHILE
THE UTILITY CINDUCTED A CHECKOUT OF
THE SCRUBBER INTERNALS AND REPLACED
SOME OF THE PACKING SPHERES IN THE
MOBILE BED.
                                                               131
                                                                            PEDCO ENVIRONMENTAL

-------
                  TABLE: 3
PERFORMANCE DESCRIPTION FOR OPERATIONAL FGD SYSTEMS  12/74
 IDENTIFICATION NO.


 UTILITY NAME


 UNIT MAKE


 UNIT LOCATION


 UNIT RATING


 FUEL CHARACTERISTICS


 FGO VENDOR


 PROCESS


 NEW OR RETROFIT


 START UP UATE


 FGD STATUS


 EFFICIENCY,
  PARTICULATES



  S02
 KEY WEST UTILITY  BOARD


 STOC .  ISLAND PLANT


 KEY WEST FLORIDA


   37 HU


 OIL    Z.H PERCENT  SULFUR


 2URN AIR SYSTEMS


 LIMESTONE SCRUBBING


 NEW


 10/72


 OPERATIONAL



 90 PERCENT



 85 PERCENT-ESTIMATED
 WATEK MAKE UP
 SLUUCiE DISPOSAL
 OPEN LOOP 2.7 GPM/MW
 UNSTABILIZED SLUUGE DISPOSED IN UNLINED POND
 UNIT COST
* 21.6/KW CAPITAL COST
 OPERATIONAL
  EXPERIENCE
 REFER TO BACKGROUND INFORMATION SECTION IN TABLE 3 OF THIS REPORT. THIS
 FGD SYSTEM HAS f3££N OPERATIONAL SINCE OCTOBER 1972. THE F3D SYSTEM HAS
 BEEN OUT OF SERVICE SINCE JANUARY 28,1975. MODIFICATIONS AND REPAIRS ARE
 CURRENTLY IN PROGRESS. SYSTEM RESTART IS STILL INDEFINITE. A CHECKOUT
 OF  ALL SYSTEM MOTORS AND PUMPS MUST BE COMPLETED BEFORE STARTUP CAN
 COMMENCE. DURING THE REPORT PERIOD THE UNIT DlO NOT OPERATE BECAUSE OF
 REPAIRS TO BOILER TUBES THAT FAILED. RESTART IS SCHEDULED SHORTLY.
                                                            132
                                                                         PEDCO ENVIRONMENTAL

-------
                                                                BACKGROUND INFORMATION



                                                                          ON




                                                                  STOCK ISLAND PLANT



     THE UTILITY BOARD OF THE CITY OF KEY WEST OWNS AND OPERATES A NEW 37-MW OIL-FIRED POWER BOILER. INSTALLED AT THEIR STOCK



ISLAND PLANT WHICH IS LOCATED DIRECTLY ADJACENT TO THE ISLAND CITY OF KEY WEST.  THE BOILER IS AN ERIE CITY BALANCED.DRAFT OIL-




FIRED UNIT THAT IS NOMINALLY RATED AT 37 MW AND CAN ACHIEVE <*2 MW AT FULL PERFORMANCE.  THE UNIT FIRES NO. 6 RESIDUAL FUEL OIL



FROM VENEZUELA UlTh SULFUR AND ASH CONTENTS OF 2.75 AND 0.05 PERCENT, RESPECTIVELY. THE UNIT'S GROSS HEAT RATE IS 11,360




BTU/KWH.  INITIAL OPERATION OF THE UNIT COMMENCED IN NOVEMBER 1972.



     THE EMISSION CONTROL SYSTEM FOR THIS UNIT CONSISTS OF A MULTIPLE TUBE MECHANICAL OUST COLLECTOR INSTALLED UPSTREAM OF TWO



SULFUR DIOXIDE WET SCRUBBERS DESIGNED AND INSTALLED BY ZURN AIR INDUSTRIES.  THIS IS A DEMONSTRATION FACILITY (EPA FUNDED)



EMPLOYING LIMESTONE  IN A SEAwATER SOLUTION FOR THE REMOVAL OF SULFUR DIOXIDE FROM THE BOILER FLUE GAS STREAM.  NO PROVISIONS FOR



STACK GAS REHEAT EXIST AT THE FACILITY.



     THE LIMESTONE ABSORBENT IS OBTAINED FROM CORAL DREDGED FROM THE OCEAN.  THE CORAL CONSISTS PRIMARILY OF CAC03 WITH LITTLE OR



NO MGC03.  THE CORAL IS GROUND TO A FINE POWDER  IN A HAMMERMILL CRUSHER TO 90 PERCENT MINUS 325 MESH AND SLURRIED IN SEAWATER.



     ZURN DUSTRAXToRS ARE EMPLOYED FOR  THE REMOVAL OF SULFUR DIOXIDE AND RESIDUAL PARTICULATES FROM THE BOILER FLUE GAS.  THE TWO



SCRUBBER MODULES ARE DESIGNED TO HANDLE A COMBINED TOTAL OF 126,950 CFM AT ISO F.  FLUE GASES FROM THE BOILER ARE DRAWN THROUGH AN



INDUCED DRAFT FAN AND FORCED EITHER THROUGH THE  BYPASS DUCT OR THROUGH ONE OR BOTH SCRUBBEKS VIA THREE SETS OF DAMPERS BETWEEN THE



.INDUCED-DRAFT FAN AND THE STACK.  BEFORE ENTERING THE SCRUBBING SYSTEM THE GAS IS COOLED FROM 360 F TO 160 F BY SEAWATER SPRAYS.



THIS COOLING PROTECTS THE FIBERGLASS COMPONENTS  OF THE SCRUBBER MODULES.  A PRESSURE DROP OF 12 TO 1H INCHES WATER GAUGE IS THE



NORrtAL OPERATING RANGE FOR THE SCRUBBERS.  THE SPENT SCRUBBING SLURRY IS BLED OFF TO TWO ON-SITE SETTLING PONDS WITH A RETENTION



CAPACITY OF 21 DAYS. THE SLUDGE SETTLES OUT AND CLARIFIED WATER IS DISCHARGED BACK INTO THE SEA BY AN OVERFLOW PIPE AND SEEPAGE.



THE PARTICULATE AND  SULFUR DIOXIDE REMOVAL EFFICIENCIES OF THE EMISSION CONTROL SYSTEM ARE 6
-------
 STOCK ISLAND (CONTINUED)



SYSTEM PERFORMANCE



     STAKT-UP OF THE SCRUBBING SYSTEM OCCURRED IN AUGUST 1973.  ENSUING OPERATION HAS PROCEEDED ON AN INTERMITTENT BASIS.  THE



MAJOR PROBLEM AREAS ENCOUNTERED HAVE INCLUDED*



     SEVERE CORROSION OF GAS QUENCH DUCT AND DAMPER SEALING FANS ON INLET AND OUTLET OF SCRUBBERS.



     PLUGGING AT THE BOTTOM OF SCRUBBER TUBES.



     LIQUID LEVEL CONTROL FAILURES IN THE SCRUBBER MODULES.



     POOR LIMESTONE UTILIZATION (APPROXIMATELY 20 PERCENT).



     INDUCED DRAFT FAN REPAIRS.



     REPLACEMENT OF INTERNAL STAINLESS STEEL PARTS WITH MONEL COMPONENTS,



     BOILER FOUNDATION AND BOILER TUBE PROBLEMS.



     LIMESTONE SUPPLY SHORTAGES.



     ADDITIONAL INFORMATION AND DETAILS ON THE PROGRESS OF THIS INSTALLATION ARE PRESENTED IN THE PERFORMANCE TABLE BELOW.  A



PROCESS FLOW DIAGRAM IS PRESENTED IN FIGURE 13 OF APPENDIX C.
                                                               134                                PEOCO ENVIRONMENTAL

-------
                                                           STOCK ISLAND (CONTINUED)

                OPERATING HOURS           FGD SYSTEM
MONTH        BOILER      FGD SYSTEM      AVAILABILITY                           COMMENTS

                                                            FGD SYSTEM WAS SHUT DOWN ON JANUARY 2fl, 1975, BECAUSE OF DAMAGED

                                                            DUCTWORK BAFFLES.  SPRAY TREES AND OTHER STAINLESS STEEL PARTS HAVE

                                                            BEEN RREPLACEO WITH MONEL.

JUL. 75                                                     FGD SYSTEM IS STILL OUT OF SERVICE BUT IS SCHEDULED FOR RESTART IN

                                                            EARLY OCTOBER.

AUG. 75                                                     BOILER HAS BEEN DOWN SINCE AUGUST 90 FOR REPAIRS OF THE INDUCED-DRAFT

                                                            FAN.

SEP. 75                                                     FGD SYSTEM IS STILL OUT OF SERVICE.  DATE OF SYSTEM RESTART IS

                                                            INOEFINTE.

OCT. 75

NOV. 75                                                     FGD SYSTEM IS STILL OUT OF SERVICE.  THE UTILITY IS REPLACING DAMPERS

DEC. 75                                                     AND VARIOUS SYSTEM PARTS.  DATE OF SYSTEM RESTART IS STILL INDEFINITE.

JAN. 76                                                     REPAIRS TO OUTLET DAMPER ARE COMPLETE.  ALL HOLES IN THE HOPPER WALL

FEB. 76                                                     AND DUCTWORK HAVE BEEN PATCHED.  NEW SpRAY TREES HAVE BEEN INSTALLED.

                                                            THE SYSTEM WILL NOT BE PLACED IN SERVICE UNTIL A THOROUGH CHECKOUT

                                                             OF ALL THE PUMPS AND MOTORS IS FIRST  COMPLETED.

MAR. 76                                                     THE FGD SYSTEM RESTART HAS BEEN DELAYED BECAUSE OF BOILER-RELATED

APR. 76                                                     PROBLEMS.  DATE OF SYSTEM RESTART IS STILL INDEFINITE.

HAY  76                                                     THE UTILITY REPORTED THAT REPAIRS AND  MODIFICATIONS ARE WEARING

                                                            COMPLETION.

JUN. 76                                                     SYSTEM RESTART IS EXPECTED SHORTLY.
                                                                135                                 PEOCO ENVIRONMENTAL

-------
                                                           STOCK  ISLAND  (CONTINUED)
                OPERATING  HOURS            FGD  SYSTEM
MONTH        BOILER     FGU  SYSTEM       AVAILABILITY                           COMMENTS
JUL. 76                                                     ALL MODIFICATIONS  TO  THE SCRUBBING  SYSTEM WHICH CAN BE MADE AT THE
AUG. 76                                                     PRESENT TIME HAVE  BEEN COMPLETED.   THE SCRUBBING SYSTEM HAS BEEN
                                                            SEALED OFF FROM  THE BOILER  BY  A  METAL PARTITION WHILE THE MODIFICA-
                                                            TIONS WERE IN PROGRESS.  FINAL MODIFICATIONS CAN BE COMPLETED ONLY
                                                            WHEN  THE  SCRUBBING SYSTEM AND  BOILER HAVE BEEN INTEGRATED INTO ONE
                                                            UNIT, WHICH  WILL REQUIRE BRINGING THE BOILER DOWN.  THE UNIT IS
                                                            CONTINUING TO FIRE 2.1-2.4  PERCENT  SULFUR FUEL OIL.
SEP. 76                                                     THE BOILER HAS BEEN TAKEN OUT  OF SERVICE BECAUSE OF TUBE FAILURES.
OCT. 76                                                     THE METAL PARTITION BETWEEN THE  SCRUBBING SYSTEM AND BOILER HAS
                                                            BEEN  REMOVED.  A SHAKE-DOWN AND  TEST RUN ON WATER WILL BE CONDUCTED
                                                            SHORTLY.
NOV. 76                                                     THE UTILITY  REPORTED  NO CHANGE IN STATUS, REPLACEMENT PARTS HAVE
DEC. 76                                                     JUST  REACHED THE PLANT. TENATTIVE RESTART DATE IS FEB. 1. 1977.
                                                              136                                PEOCO ENVIRONMENTAL

-------
                  TABLE 3
PERFORMANCE DESCRIPTION FOR OPERATIONAL F60 SYSTEMS  12/76
 IDENTIFICATION NO.

 UTILITY NAME

 UNIT NAME
 UNIT LOCATION

 UNIT RATING

 FUEL CHARACTERISTICS

 FGO VENDOR

 PROCESS

 NEW OR RETROFIT

 START UP DATE

 FGO STATUS

 EFFICIENCY,
  PARTICULATES
 LOUISVILLE  GAS &  ELECTRIC

 CANE  RUN NO 
-------
                                                           BACKGROUND INFORMATION



                                                                     ON



                                                               CANE RUN NO.  4



     THE CANE RUN POWER  STATION  IS  OPERATED BY  THE LOUISVILLE GAS AND ELECTRIC COMPANY AND LOCATED IN LOUISVILLE*  KENTUCKY.  THE



PLANT CONSISTS OF SIX  ELECTRIC POWER  STEAM GENERATING UNITS HAVING A TOTAL STEAM TURBINE NET GENERATING CAPACITY OF 992-MW.



     UNIT NO. H IS A COAL-FIRED  STEAM GENERATING BOILER WITH A CONTINUOUS NET GENERATING CAPACITY OF 17S-MW.   THE UNIT HAS A




MAXIMUM POWER GENERATION CAPACITY OF  190-MW. THE UNIT HEAT RATE IS 10,030 BTU/KWH.   THE BOILER IS CURRENTLY  BURNING COAL WITH A



GROSS HEATING VALUE OF 11,500 BTU/LB  AND AVERAGE SULFUR AND ASH CONTENTS OF 3.5-H.O  PERCENT AND 11.0-12.0 PERCENT, RESPECTIVELY.



     THE EMISSION CONTROL SYSTEM FOR  THIS UNIT  CONSISTS OF AN ELECTROSTATIC PRECIPITATOR (ESP)  UPSTREAM OF A  WET SCRUBBING SYSTEM.



THE ESP PROVIDES PRIMARY PARTICULATE  CONTROL WHILE THE WET SCRUBBING SYSTEM PROVIDES ADDITIONAL PARTICULATE REMOVAL AND PRIMARY



SULFUR DIOXIDE CONTROL.



     THE FLUE GAS DESULFURIZATION  (FGD)  SYSTEM  CONSISTS OF TWO IDENTICAL PARALLEL SCRUBBING TRAINS DESIGNED AND INSTALLED BY THE



AMERICAN AIR FILTER (AAF) COMPANY.   THE WET SCRUBBING SYSTEM UTILIZES A SLURRY OF CARBIDE LIME FOR SULFUR DIOXIDE REMOVAL FROM THE



FLUE GAS.  THE CARBIDE LIME IS  A WASTE BY-PRODUCT OBTAINED FROM A NEARBY ACETYLENE MANUFACTURING PLANT.  THE  HYDRATED LIME CON-



TAIfJS 90.0 TO 92.0 PERCENT CALCIUM HYDROXIDE, 2.0 TO 2.5 PERCENT SILICA, 3.0 TO 8.0  PERCENT CALCIUM CARBONATE, AND 0.1 PERCENT



MAGNESIUM OXIDE.



     EACH SCRUBBING TRAIN IS EQUIPPED WITH A GUILLOTINE-TYPE BY-PASS DAMPER ALLOWING BY-PASSING OF THE GAS AROUND THE SCRUBBERS.



EACH SCRUBBING TRAIN CONTAINS THE FOLLOWING MAJOR PIECES OF EQUIPMENT*  1.0. BOOSTER FAN, QUENCH SECTION, FLOODED ELBOW, MOBILE



BED CONTACTOR, CENTRIFUGAL OEMISTER, AND A 3-SECTION REACTANT TANK SYSTEM.  THE WASTE DISPOSAL SYSTEM CONSISTS OF A 75-FOOT



DIAMETER THICKENER FOR LIQUID-SOLIDS SEPARATION AND A FLY ASH POND FOR ULTIMATE DISPOSAL OF THE THICKENER UNDERFLOW.  THE SCRUB-



BING WASTES ARE STABILIZED WITH FLY ASH AND WATER IS RECYCLED BACK TO THE PROCESS. THE SYSTEM DOES NOT USE A  STACK GAS REHEAT



SYSTEM.  A WET STACK.  WHICH IS  THE EXISTING STACK LINED WITH CARBOLYNE, OBVIATES THE NECESSITY OF REHEAT.
                                                               138                                PEOCO ENVIRONMENTAL

-------
                                                           F60 SYSTEM PERFORMANCE

                                                            CANE RUN UNIT NO. 
-------
                                                           FSO SYSTEM PERFORMANCE

                                                            CANE RUN UNIT NO.  H

                                                PERFORMANCE FACTORS (X)
PERIOD   HOURS   BOILER (HR)   SCRUBBERS (HR)    OPERABILITY   UTILIZATION                                 COMMENTS

                                                                           OF  THE SYSTEM,  AS A FUNCTION OF SERVICE TiME VERSUS

                                                                           OUTAGE TIME,  HAS BEEN VERY GOOD.

NOV. 76   720                                      95                      THE SYSTEM INCURRED NO MAJOR PROBLEMS OR UPSETS

DEC. 76   711                                      90                      DURING THE REPORT PERIOD.  CARBIDE LIME SLURRY IS

                                                                           EMPLOYED AS THE SULFUR DIOXIDE ABSORBENT.
                                                               1UO                                PEDCO ENVIRONMENTAL

-------
                  TABLE 3
PERFORMANCE DESCRIPTION FOR OPERATIONAL F60 SYSTEMS  12/76
 IDENTIFICATION NO.

 UTILITY NAME

 UNIT NAME

 UNIT LOCATION

 UNIT RATING

 FUEL CHARACTERISTICS

 F6D VENDOR

 PROCESS

 NEW OR RETROFIT

 START UP DATE

 F6D STATUS

 EFFICIENCY,
  PARTICULATES
  56

 LOUISVILLE 6AS & ELECTRIC

 PADDYS RUN NO 6

 LOUISVILLE KENTUCKY

   65 MM

 COAL  3.5-1.0 PERCENT SULFUR

 COMBUSTION ENGINEERING

 LIME SCRUBBING

 RETROFIT

  H/73

 OPERATIONAL


 99 PERCENT  DESIGN
  S02
 80 PERCENT (DESIGN)
 WATER MAKE UP
 SLUDGE DISPOSAL
 UNIT COST
 OPERATIONAL
  EXPERIENCE
 OPEN LOOP 0*7 GPM/MU
 UNSTABILIZED SLUDGE DISPOSED IN UNLINED POND
S57/KW CAPITAL
2.5 MILLS/KWH OPERATING
 REFER TO THE BACKGROUND INFORMATION SECTION IN TABLE 3 OF THIS REPORT.
 THIS SCRUBBING SYSTEM UAS DESIGNED BY  COMBUSTION ENGINEERING AND PLACED
 IN SERVICE IN APRIL 1973. PADDYS RUN NO.6 IS A PEAK-LOAD UNIT THAT
 OPERATES ONLY DURING DEMAND PERIODS.  THE UNIT WAS OPERATIONAL DURING
 THE REPORT PERIOD*  BEING AVAILABLE TO  THE BOILER ON 99 PERCENT BASIS.
 SCRUBBER OPERATIONS WERE CONDUCTED ON  CARBIDE LIME SLURRY DURING THE
 PERIOD.  THE EPA-SUBSIOIZED SCRUBBER/SLUDGE STUDY CALLS FOR A HIGH
 CALCIUM VIRGIN LIME RUN TO COMMENCE ON MARCH It 1977.
                                                                                               PEDCO ENVIRONMENTAL

-------
                                                               BACKGROUND INFORMATION



                                                                          ON



                                                              PADDY'S RUN POWER STATION



     PADDY'S RUN POWER STATION IS LOCATED IN LOUISVILLE, KENTUCKY.  THE PLANT HAS SIX ELECTRIC POWER GENERATING UNITS WITH A TOTAL



RATED CAPACITY OF 320 MW. UNIT NO. 6 IS RETROFITTED WITH A CARBIDE LIME-BASE FGD SYSTEM.



     UNIT NO. 6 IS A PEAK LOAD COAL-FIRED BOILER, MANUFACTURED BY FOSTER WHEELER AND INSTALLED IN 1950.  THIS UNIT FIRES COAL WITH



A GROSS HEATING VALUE OF 11,500 BTU/LB AND AVERAGE SULFUR AND ASH CONTENTS OF 3.7 PERCENT AND 13 PERCENT, RESPECTIVELY.



     THE FGD SYSTEM CONSISTS OF TWO MODULES.  EACH HANDLES 175,000 ACFM OF sso F FLUE GAS.  EACH MODULE is MADE UP OF TWO STAGES



OF 3-INCH MARBLE BEDS, FOLLOWED BY A TWO-STAGE CHEVRON-TYPE OEMISTER.  THE GAS IS REHEATED BY DIRECT COMBUSTION OF NATURAL GAS.



SCRUBBING SYSTEM PROVIDING PRIMARY CONTROL OF PARTICIPATE EMISSIONS. THIS UNIT OPERATES WITH A 99.1 PERCENT PARTICULATE REMOVAL



EFFICIENCY. PARTICULATE LOADING AT THE ESP OUTLET IS 0.05 GR/SCF



PARTICULATE LOADING AT THE ESP OUTLET IS 0.05 GR/SCF.



     THE SYSTEM UTILIZES A SLURRY OF CARBIDE LIME AS THE SULFUR DIOXIDE ABSORBENT.  THE CARBIDE LIME, A WASTE BY-PRODUCT OBTAINED



FROM A NEARBY ACETYLENE MANUFACTURING PLANT CONTAINS 90 TO 92.0 PERCENT CALCIUM HYDROXIDE, 2.0 TO 2.5 PERCENT SILICA, 3.0 TO 6.0



PERCENT CALCIUM CARBONATE, AND 0.1 PERCENT MAGNESIUM OXIDE.



     THE UNIT OPERATES ON A CLOSED-LOOP MODE*  THE SULFUR DIOXIDE IS ABSORBED IN THE MARBLE BED BY A SLURRY OF CALCIUM SULFITE TO



FORM A MIXTURE OF  CALCIUM SULFITE/BISULFITE.  EFFLUENT FROM THE MARBLE-BED TOWER IS CONVERTED IN THE REACTION TANK TO CALCIUM



SULFITE BY  THE ADDITION  OF CALCIUM HYDROXIDE.  HALF OF THE REACTION TANK EFFLUENT IS RETURNED TO THE ABSORBER TOWERS WHILE THE



OTHER HALF  IS FED  TO  A CLARIFILR  TANK.  THE CALCIUM SULFITE CRYSTALS PRECIPITATE WITH THE AID OF A FLOCCuLANT. WHICH IS ADDED AT



THE RATE OF H TO 7 PPM.  THE  OVERFLOW  is RETURNED TO THE REACTION TANK.  THE UNDERFLOW, CONTAINING 22 TO 2«t PERCENT SOLIDS, is



STABILIZED  BY MIXING  IT  WITH  LIME.   APPROXIMATELY 60 TO 100 POUNDS OF LIME ARC USED PER TON OF DRY SOLIDS OF SLUDGE.  THE FIXED



SLUDGE IS TRANSPORTED BY TRUCKS TO A 10-ACKE OFF-SITE LANDFILL AREA.



     DURING THE INITIAL 45 DAYS OF OPERATION ONLY ONE ABSORBER WAS PLACED IN SERVICE, ALLOWING OPERATORS TO OBSERVE THE EQUIPMENT



AND TO DETERMINE ANY NEEDED MODIFICATIONS.  BEGINNING MAY 19, 1974, THE SYSTEM WAS SHUT DOWN FOR A MONTH FOR MODIFICATIONS, THE



MOST SIGNIFICANT BEING INSTALLATION OF EQUIPMENT FOR INJECTING A FLOCCULATING AGENT INTO THE CLARIFIER TANK.  DURING THE PERIOD



JUNE 19 TO JULY 11, INCONSISTENT SIZING OF SLURRY ADDITIVE MATERIAL AS RECEIVED CAUSED MALFUNCTION OF THE ADDITIVE CONTROL VALVES



AND UNDUE PLUGGING OF SLURRY LINE STRAINERS.  THESE PROBLEMS WERE CORRECTED BY INSTALLATION OF A DISINTEGRATOR IN THE SLURRY










                                                                                                  PEOCO ENVIRONMENTAL

-------
PADDY'S NUN (CONTINUED)



MODIFICATION HADE WAS LOWERING THE SLURRY PH TO REMOVE SULFITE SCALE FORMATION ON THE UPPER BED PERFORATED SUPPORT PLATE AND ON




MODIFICATION MADE WAS LOWERING OF THE SLURRY PH TO REMOVE SULFITE SCALING FORMED ON THE UPPER BED PERFORATED SUPPORT PLANT AND ON




THE MARBLES*
                                                                                                  PEOCO ENVIRONMENTAL

-------
MONTH

APR. 75



MAY  73





JUN, 73



JUL. 73





AUG. 73
SEP. 73



OCT. 73

OCT9 73

NOV. 73

OEC. 73

JAN. 74

THROUGH

JUL. 7«
  OPERABILITY (X)
MODULE A  MODULE B

  18        56
  11
  21
  53
 21
  65
 72
  35
104

 7fl

  0
                             F60 SYSTEM OPERABILITY

                             PADDY'S RUN UNIT NO. 6


                                   COMMENTS

MODULES WERE OPERATED ONE AT A TIME, WITH FREQUENT SHUTDOWNS FOR INSPECTION OF EQUIPMENT AND

MINOR REPAIRS.

SINGLE-MODULE OPERATION CONTINUED THROUGH MAY 19, WHEN THE UNIT WAS SHUT DOWN FOR MODIFICA-

TIONS.  THE MOST SIGNIFICANT MODIFICATION WAS INSTALLATION OF EQUIPMENT FOR INJECTION OF A

FLOCCULATING AGENT INTO THE CLARIFIER TANK.

OPERATION MAS INTERMITTENT FROM JUNE 19 TO JULY 11 BECAUSE OF MECHANICAL PROBLEMS WITH THE

SLURRY PUMPS.

DURING A SCHEDULED OUTAGE FROM JULY 12 THROUGH AUGUST 1« SEVERAL REPAIRS WERE MADE TO THE LINE

SLURRY MAKEUP SYSTEM.  A DISINTEGRATOR UNIT WAS INSTALLED TO REDUCE PLUGGING OF STRAINERS AND

SLURRY CONTROL VALVES.

THE OPERATION WAS CONTINUOUS FROM AUGUST 2 TO AUGUST 18 EXCEPT FOR A BRIEF SHUTDOWN DUE TO A

BOILER-RELATED PROBLEM.  FROM AUGUST 19 TO SEPTEMBER 5t THE SYSTEM WAS SHUT DOWN TO REPLACE THE

CLARIFIER'S UNDERFLOW LINE WITH ONE OF LARGER DIAMETER AND TO INSTALL ADDITIONAL PUMP CAPACITY

IN THE CLARIFIER«S OVERFLOW SYSTEM.

THE UNIT OPERATED CONTINUOUSLY BETWEEN SEPTEMBER 6 AND SEPTEMBER 20 EXCEPT FOR A 7-HOUR SHUT-

DOWN TO REPAIR A MARBLE BED SUPPORT PLATE.  THE UNIT WAS SHUT DOWN THE REMAINDER OF THE MONTH

THE FGO SYSTEM REMAINED IN SERVICE TO DEC. 20 AFTER WHICH THE BOILER AND THE SCRUBBER MODULES

THE FbQ SYSTEM WAS IN SERVICE THROUGH DECEMBER 20 AFTER WHICH THE BOILER (AND THE SCRUBBERS)

WERE SHUT DOWN BECAUSE 0F *No DEMAND* (THIS IS A PEAKING-LOAD BOILER).



BOILER SHUT DOWN BECAUSE OF *NO DEMAND**
                                                                                                  PEDCO ENVIRONMENTAL

-------
MONTH
AUG. 7«*
SEP. 7«t
OCT. 7«»
NOV. 7H
THROUGH
AUG. 75
SEP. 75
OCT. 75
NOV. 75
DEC. 75

JAN. 76
FEB. 76
  OPERABILITY (X)
MODULE A  MODULE B
  50
   0
 100
 NO DEMAND
 77
  0
100
 100
 100
100
 100
 100
  90
100
 90
 100       100
 NO DEMAND
                             FGO SYSTEM OPERABILITY
                             PADDY'S RUN UNIT NO. 6

                                   COMMENTS
UNIT HAS BEEN ON AND OFF FREQUENTLY DUE TO FLUCTUATION IN POWER DEMAND.
BOILER IS DOWN BECAUSE OF *NO DEMAND.*
BOILER TURNED ON SPECIFICALLY TO PERFORM LIMESTONE TESTS ON FGD SYSTEM.
BOILER IS DOWN BECAUSE OF *NO DEMAND.*
BOILEK AND FGD SYSTEM OPERATIONAL ALL OF SEPTEMBER AND FIRST TWO WEEKS IN OCTOBER.  SYSTEM
OUTAGE DURING THE LAST TWO WEEKS OF OCTOBER WAS DUE PRIMARILY TO BREECHING IN THE BOILER
SECTION.  OPERABILITY FOR BOTH MODULES DURING THE OPERATIONAL PERIOD WAS 100 PERCENT (BASED
UPON LG&E«S PEAK LOAD DETERMINATION).  S02 REMOVAL WAS REPORTED TO BE OyER 98 PERCENT.
BOILER AND SCRUBBER SYSTEM RAN MOST OF THE REPORT PERIOD ON A MONDAY-THROUGH-FRIDAY BASIS..  TWO
MINOR OUTAGES IN DECEMBER WERE DUE TO MALFUNCTION AND REPAIR OF THE DUAL STRAINER SWITCH SHAFT
IN THE BOTTOM OF THE SCRUBBER MODULE.
502 REMOVAL EFFICIENCY WAS REPORTED TO BE 99 PERCENT DURING JANUARY.  THE SYSTEM WAS SHUT DOWN
IN EARLY FEBRUARY IN PREPARATION FOR AN EPA SCRUBBER/SLUDGE STUDY SCHEDULED FOR JUNE OR JULY.
THE SCRUBBER WILL NOT BE OPERATED UNTIL THE START OF THE STUDY PROGRAM UNLESS THE BOILER IS
REQUIRED FOR PEAKING POWER DEMANDS.  HIGHLIGHTS OF THE SCRUBBER/SLUDGE STUDY PROGRAM ARE AS
FOLLOWS*
     6 MONTH DURATION.
     ONE SCHEDULED SHUTDOWN FOR TEST MODIFICATIONS.
                                                               1*5
                                                                                     .REDCO ENVIRONMENTAL

-------
MONTH
MAR. 76

APR. 76

KAY 76

JUN. 76
JUL. 76

AUG. 76



SEP. 76

OCT. 76
NOV. 76

DEC. Tfr
  OPEKABILITY (X)
MODULE A  MODULE B
   NO DEMAND

   NO DEMAND

100        10&

100        100
190

100
180

100
   NO DEMAND
 99

 99
 99

 99
                             FGD SYSTEM OPERABILITY

                             PADDY'S RUN UNIT NO. 6


                                   COMMENTS

     DELIBERATE HIGH CHLORIDE CONCENTRATION OPERATION.

     MGO INNOCULATION.

     EXTENSIVE SLUDGE STUDY*  FIXATION* LEACHATES. SEASONAL VARIATIONS.

THE UNIT DID NOT OPERATE DURING THE REPORT PERIOD IN ANTICIPATION OF THE EPA SCRUBBER/SLUDGE

STUDY.  THE UTILITY IS NOW COMPLETING SYSTEM MODIFICATIONS FOR THE OPERATION OF THE TEST

PROGRAM.  THIS PEAK LOAD UNIT WAS OPERATED PART OF THE TIME DURING THE REPORT PERIOD (APPROXI-

MATELY 2 WEEKS IN MAY AND 2 WEEKS IN JUNE).  THE SCRUBBER WAS AVAILABLE TO THE BOILER 100

PERCENT OF THE TIME.  S02 REMOVAL EFFICIENCY WAS 98 TO 99 PERCENT DURING THIS OPERATING SEG-

MENT.  THE EPA-SPONSORED SCRUBBER/SLUDGE STUDY IS NOW SCHEDULED TO COMMENCE SEPTEMBER 1* 1976.

THE UNIT WAS OPERATIONAL PART OF THE TIME DURING THE JULY-AUGUST PERIOD.  THE SCRUBBING SYSTEM

WAS AVAILABLE TO THE BOILER ON A 100 PERCENT BASIS*  NO MAJOR SCRUBBER-RELATED PROBLEMS W£RE

ENCOUNTERED.

THE UNIT DID NOT OPERATE THROUGHOUT SEPTEMBER AND THE FIRST 3 WEEKS OF OCTOBER.

THE EPA-FUNDED SCRUBBER/SLUDGE STUDY PROGRAM COMMENCED OCTOBER 25.  THE INITIAL PHASE OF

THE PROGRAM CALLS FOR OPERATIONS TO PROCEED FOR A 20 TO- 30-OAY PERIOD WITH CARBIDE LIME

SCRUBBING ABSORBENT.  FOLLOWING COMPLETION OF THIS RUN* THE UNIT WILL BE SHUT DOWN AND

MODIFICATIONS WILL  BE INCORPORATED INTO THE SYSTEM FOR OPERATION WITH COMMERCIAL GRADE (HIGH

CALCIUMI LIME.

THC ufoiT WAS IN SERVICE DURING* THE REPORT PERIOD. THE SCRUBBING SYSTEM OPERATED 99.5 PERCENT

Of THE TIME THE BOILER WAS IN SERVICE. CARBIDE LIME WAS EMPLOYED AS THE 502 ABSORBENT. THE

HI6++ CALCIUM {VIRGIN) LIME RUN, SCHEDULED AS PART OF THE SCRUBBER/SLUDGE STUDY* WILL COMMENCE

OW MARCH It 1977.
                                                               1*6
                                                                                     PEOCO ENVIRONMENTAL

-------
                  TABLE 3
PERFORMANCE DESCRIPTION FOR OPERATIONAL FGO SYSTEMS  12/76
 IDENTIFICATION NO.
 UTILITY NAME
 UNIT NAME
 UNIT LOCATION
 UNIT HATING
 FUEL CHARACTERISTICS
 FGD VENDOR
 PROCESS
 NEW OR RETROFIT
 START UP DATE
 FGD STATUS
 EFFICIENCY.
  PARTICULATES
  59
 MONTANA POWER CO.
 COLCTRIP NO 1
 COLSTRIP MONTANA
  360 MU
 COAL   0.8 PERCENT SULFUR
 AOL/COMBUSTION EQUIP ASSOCIATE
 LIME/ALKALINE FLYASH SCRUBBING
 NEW
 10/75
 OPERATIONAL

 99 PERCENT
  S02
 60 PERCENT
 UATEK MAKE UP
 SLUDGE DISPOSAL
 UNIT COST
 CLOSED LOOP
 UNSTABILIZED SLUDGE DISPOSED IN UNLINED POND
$50/Kh CAPITAL
 OPERATIONAL
  EXPERIENCE
 THE COLSTKIP PLANT IS A MINE MOUTH INSTALLATION.  CONSTRUCTION ON THIS
 UNIT WAS COMPLETED BEHIND SCHEDULE.  THE FGD SYSTEM STARTED UP IN LATE
 1975 AND PROCEEDED THROUGH A SHAKEDOWN AND DEBUGGING OPERATION PHASE. THE
 UMT HAS BEEN OPERATING AT FULL COMMERCIAL CAPACITY.  THE SCRUBBING
 SYSTEM DESIGN INCORPORATES THE VENTURI WET SCRUBBERS FOR PARTICULATE
 AND SULFUR DIOXIDE REMOVAL.  FLUE GAS CANNOT BE BYPASSED AROUND THE
 SCRUBBING SYSTEM.  INFORMATION AND OPERATING DATA WERE NOT MADE
 AVAILABLE BY THE UTILITY DURING THE REPORT PERIOD.
                                                                                               PEOCO ENVIRONMENTAL

-------
                  TABLE 3
PERFORMANCE DESCRIPTION FOR OPERATIONAL F6D SYSTEMS   12/76
 IDENTIFICATION NO.

 UtILffY NAME

 UN ft NAM£

 UNIT LOCATION

 UNIT RATIN6

 FUEL CHARACTERISTICS

 FGD VENDOR

 PROCESS

 NEW OR RETROFIT

 START UP DATE

 FGD STATUS
  PARfiCULATES
 60F

MONTANA POWER CO.

COL^fRIP W0 2

COLSTRIP MONTANA

 36$ MW

Cm   6<& WttCENt SULFUtf

AOL/COMBUST ION- EQUIP ASSOCIATE,

LIHE/AtKACfNE FLYASH SCRUBS INS

NEW

 7/76

OPERATIONAL


99 PERCENT
  SO?


 WATER HAKE- UP


 SLUDGE


 UNiT COST
 OPER'A'fKJNA'L
  EXPERIENCE
CLOSES LOOP1
             SLUDGE DISPOSED IN UNLlNtD POND
      CAPltAtr
    C^fcS-fRlP  PLANT  IS A MINE MOUTH FA(iIL*Ty. CONSTRUCTION OF THE FGO
       H*&  B6.EM COMPLETED«  TURrflNE ROLL AND &YSTEH CHECI OUT HAVE BEEN
            iNitlM  OP£R^fl6N OF THE SCRUBBINS SYSTEM COMMENCED IN
     i*t"6.  fHIS UNlf iS IDENTICAL TO fn£ NO.i SYSTEM OESlSN IN THAT
      SCWJB6ER  HODULES ARE  INSTALLED I^OR PARTICULATE AND SULFUR DIOXIDE
REMOVAL. FLUE GAS CONAOT BE BY-PASSED AROUND THE SCRUBBING SYSTEM.
            ANO OPEPfAflWS DATA MfRC NflPt MADE AVAILABLE BY THE UTILITY
       THE  REPORT PERIOo.
                                                             ins
                                                                         PCDCO £NVIRONMEJVTAt

-------
                  TABLE 3
PERFORMANCE DESCRIPTION FOR OPERATIONAL FGD SYSTEMS  12/76
 IDENTIFICATION NO.
 UTILITY NAME
 UNIT NAME
 UNIT LOCATION
 UNIT HATING
 FUEL CHARACTERISTICS
 FGO VENDOR
 PROCESS
 NEW OR RETROFIT
 START UP DATE
 FGD STATUS
 EFFICIENCY.
  PARTICULATES
 67
NEVADA POWER
RE III- GARDNER NO 1
nOAPA NEVADA
 125 MW
COAL   0.5- 1.0 PERCENT SULFUR
AOL/COMBUSTION EQUIP ASSOCIATE
SODIUM CARBONATE SCRUBBING
RETROFIT
OPERATIONAL

99 PERCENT
  S02
85 PERCENT
 WATER HAKE UP
 SLUU6E DISPOSAL
OPEN LOOP 1.52 GPH/MW
UNSTABILIZLD SLUDGE DISPOSED IN UNLINED POND
 UNIT COST
 OPERATIONAL
  EXPERIENCE
      CAPITAL (197
-------
                  TABLE 3
PERFORMANCE DESCRIPTION FOR OPERATIONAL F6D SYSTEMS  12/76
 IDENTIFICATION NO.


 UTILITY NAME


 UNIT NAME


 UNIT LOCATION


 UNIT RATING


 FUEL CHARACTERISTICS


 FGD VENDOR


 PROCESS


 NEW OR RETROFIT


 START UP DATE


 FGO STATUS


 EFFICIENCY,
  PARTlCULATES



  S02



 WATER MAKE UP



 SLUDGE DISPOSAL



 UNIT COST



 OPERATIONAL
  EXPERIENCE
 68


NEVADA POWER


REIL' GARDNER NO 2


nOAPA NEVADA


 125 MU


COAL   0.5- 1.0 PERCENT SULFUR


AOL/COMBUSTION EQUIP ASSOCIATE


SODIUM CARBONATE SCRUBBING


RETROFIT
OPERATIONAL



99 PERCENT



85 PERCENT



OPEN LOOP  1.52 GPH/MW



UNSTABILIZED  SLUoGE DISPOSED  IN UNLINEQ PONo



           OOLLAKSJ* JC600 «600ANNUALlZEO
REFER TO THE BACKGROUND  INFORMATION SECTION IN TABLE 3 OF THIS REPORT.
THIS SODIUH CARBONATE-BASED  (TRONA) SCRUBBING SYSTEM CONSISTS OF ONE
MOGULS CONTAINING A TwIN VARIABLE-THKOAT VENTURI SCRUBBER FOLLOWED BY A
SIN9l£«STAGE PERFORATED-PLATE WASHING TOWER*  THE SCRUBBING TRAIN WAS
FIRST PLACED IN THE GAS PATH IN APRIL i974.  SYSTEM OPERATION DURING THE
REPORT PERIOD WAS INTERMITTENT BECAUSE OF SCRUBBER AND BOILER-RELATED
PROBLEMS.
                                                            150
                                                                        PEDCO ENVIRONMENTAL

-------
                  TABLE 3
PERFORMANCE DESCRIPTION FOR OPERATIONAL FGO SYSTEMS  12/76
 IDENTIFICATION NO.

 UTILITY NAME

 UNIT NAME

 UNIT LOCATION

 UNIT RATING

 FUEL CHARACTERISTICS

 FGD VENDOR

 PROCESS

 NEW OR RETROFIT

 START UP DATE

 FGD STATUS

 EFFICIENCY,
  PARTICULATES
 69

NEVADA POWER

REI- GARDNER NO 3

MOAPA NEVADA

 125 MM

COAL   0.5- 1.0 PERCENT SULFUR

ADL/COMBUSTION EQUIP ASSOCIATE

SODIUM CARBONATE SCRUBBING

NEW

 7/76

OPERATIONAL


99 PERCENT
  S02
 WATER MAKE  UP
 SLUUGE DISPOSAL
85 PERCENT
OPEN LOOP  1.52 GPM/MW
UNSTABILIZED SLUDGE DISPOSED IN UNLINED PONO
 UNIT COST
  OPERATIONAL
  EXPERIENCE
REFER TO THE BACKGROUND INFORMATION SECTION IN TABLE 3 OF THIS REPORT.
THIS UNIT  IS A NEW COAL-FIREO BOILER THAT IS EQUIPPED WITH SODIUM
CARBONATE-8ASED(TRONA>SCRUBBIN6 SYSTEM WHICH INCORPORATES A TWIN
VAKIABLE-THROAT VENTURI SCRUBBER FOLLOWED BY A SINGLE-STAGE PERFORATED-
PLATE WASHING TOWER FOR THE CONTROL OF PARTICULATES AND SULFUR
DIOXIDE.   THE BOILER COMMENCED OPERATIONS IN APRIL 1976 AND THE
SCRUBBER WAS PLACED IN SERVICE THREE MONTHS LATER.  THE SYSTEM
WAS IN SERVICE THROUGHOUT THE REPORT PERIOD*
                                                            151
                                                                        PEOCO ENVIRONMENTAL

-------
                                                     BACKGROUND INFORMATION
                                                                ON
                                                 RE.ID GARDNER UNITS 1. 2, AND 3
     THE REID GARDNER POyER STATION IS LOCATED NEAR NOAPA, NEVADA, ABOUT 50 MILES NORTH OF LAS VEGAS.  THE STATION HAS, THREE
ELECTRIC POWER GENERATING UNITS, (REID GARDNER 1, 2, AND 3) EACH RATED AT 125 MW.  UNITS 1 AND 2 ARE RETROFITTED WITH SODIUM
CARBONATE-BASED F&D SYSTEMS.  UNIT NO. 3 IS A NEW INSTALLATION, ALSO EQUIPPED WITH A SODIUM CARBONATE BASED FGO SYSTEM.  THE COAL
BURNED AT THE PLANT HAS AN AVERAGE GROSS HEATING VALUE OF 12,450 BTU/LB* AND ASH AND SULFUR CONTENTS OF 6 AND 0.5 PERCENT RESPEC-
TIVELY.
     THE FGD SYSTEMS INSTALLED ON REID GARDNER UNITS 1,2, AND 3 WERE DESIGNED AND INSTALLED BY COMBUSTION EQUIPMENT ASSOCIATES IN
ASSOCIATION WITH A.D. LITTLE.  THE SYSTEMS FOR UNITS 1 AND 2 WERE PLACED IN SERVICE IN APRIL 197 STORAGE AND SAND REMOVAL SERVES ALL THE FGD MODULES AT THE REID
GARDNER PLANT.  SULFUR DIOXIDE REMOVAL EFFICIENCY is REPORTED TO BE as PERCENT.  PRIMARY PARTICULATE REMOVAL is ACCOMPLISHED BY 75
PERCENT EFFICIENT  MERCHANICAL COLLECTORS INSTALLED UPSTREAM OF THE WET SCRUBBERS,  THE TOTAL PARTICULATE REMOVAL EFFICIENCY OF THE
.MECHANICAL  COLLECTION AND  WET SCRUBBING SYSTEM EXCEEDS THE 99 PERCENT LEVEL.
      IN THIS  SODIUM  CARBONATE PROCESS, HOT FLUE  GAS FROM THE BOILER PASSES FIRST THROUGH THE MECHANICAL COLLECTORS WHERE PRIMARY
PARTICULATE REMOVAL  TAKES  PLACE.  PRESSURE is THEN BOOSTED BY AN  INDUCED DRAFT FAN BEFORE THE GAS STREAM SPLITS AS IT ENTERS THE
TWIM-THROAT VENTURI  SCRUBBER.   THE HOT FLUE GAS  is QUENCHED BY A  SHOWER OF CIRCULATED SODIUM BASE LIQUOR*  THE GAS THEN ENTERS THE
WASH TRAY AND BUBBLES THROUGH THE RADIAL-VANE MIST ELIMINATOR, WHERE  TH£ REMAINING LIQUID DROPLETS CARRIED OVER WITH THE GAS ARE
TRAPPED AND REMOVED.
     EFFLUENT FROM THE FGO SYSTEM IS FROM TWO SOURCES*  THE SLIP  STREAM OF SPENT LIQUOR DISCHARGED FROM THE RECIRCULATION TANK,
AND THE ALKALINE CLARIFIES UNDERFLOW, WHICH SERVES TO NEUTRALIZE  THE PH OF THE COMBINED LIQUOR BEFORE IT IS DISCHARGED TO THE
                      t
SLUDGE SETTLING PONOS.  THE SPENT LIQUOR IS PUMPED INTO ONE OF TWO SETTLING PONDS.  THE OVERFLOW FROM THIS POND IS PUMPED TO A
LARGER 4&-ACRE PONbt WHERE THE BRINE IS EVAPORATED.  THE F6D SYSTEM OPERATES ON AN OPEN WATER LOOP WITH NO LIQUOR RECYCLED TO THE


                                                               152                                PEDCO ENVIRONMENTAL

-------
REID GARDNER UNITS It 2, AND 3 (CONTINUED)



MODULES FROM THE PONDS.



     ADDITIONAL INFORMATION CONCERNING THE PERFORMANCE OF THE SCRUBBERS INSTALLED AT THE REID GARDNER STATION,  INCLUDING PROBLEMS,



SOLUTIONS, AND MODIFICATIONS, ARE PRESENTED IN THE FOLLOWING TABLES.  IN ADDITION, A GENERAL PROCESS FLOW DIAGRAM OF THE SODIUM




CARBONATE SCRUBBING SYSTEM IS PRESENTED IN FIGURE 15 OF APPENDIX C.
                                                                153                                PEDCO ENVIRONMENTAL

-------
                                                               REID GARDNER 1
PERIOD



MAR. 75

APR. 75

NAY  75

JUN. 75
        BOILER
TOTAL  OPERATION
(HR.)    (HR.)
                HR.
              CALLED
AVAILABILITY  UPON TO
   (HR.)      OPERATE
OPERATION
  (HR.)
 JUL.  75

 AUG.  75

 SEP.  75    720       716

 OPERABILITY  = 76%

 UTILIZATION  s 78S

 OCT.  75    7
-------
                                                         REIO GARDNER 1 (CONTINUED)
PERIOD
        BOILER
TOTAL  OPERATION
(HR.)    (HR.)
JAN. 76    744      6«f7

AVAILABILITY = 81X

OPERABILITY = 29X

RELIABILITY = 57X

UTILIZATION = 25X

FEB. 76    696      66H

AVAILABILITY = 91%

OPERABILITY = 78X

RELIABILITY = 89X

UTILIZATION = 75X

MAR. 76    7
-------
                                                         REID GARDNER 1 (CONTINUED)
                  bOlLCR
          TOTAL  OPERATION
          (HR.)    CHR.)
PERIOD

HAT  76
JUN. 76
JUL. 76
AUG. 76    7HH
AVAILABILITY = 97*
OPERABILITY s 75*
RELIABILITY = 9**
UTILIZATION s H9*
SEP. 76    720
AVAILABILITY »9S»
OPERABILITY 4 97*
RELIABILITY s 99K
UTILIZATION = 89X
OCT. 76    7H1
AVAILABILITY »96*
OPERABILITY = 96*
RELIABILITY « 98)1
UTILIZATION * »7»
                     *79
                    656
                    670
                HR.
              CALLED
AVAILABILITY  UPON TO
   (HR.)      OPERATE
        OPERATION
          (HK.)
   719
366
360
   683
676
 639
    726
661
 6«8
                         COMMENTS

THE NO. 1 UNIT WAS SHUT DOWN THE ENTIRE MONTH FOR A SCHEDULED
TURBINE OVERHAUL AND BURNER LINE CONDUIT REPLACEMENT.
THE NO. I UNIT REMAINED OUT OF SERVICE THROUGHOUT THE MONTH FOR
COMPLETION OF THE TURBINE AND BOILER OVERHAUL WHICH COMMENCED THE
PRECEDING MONTH.
TWO FORCED SCRUBBER OUTAGES OCCURRED DURING THE MONTH ATTRIBUTED
TO PLUGGING IN THE TRAY RECYCLE TANK AND THICKENER TANK.  TOTAL
BOILER OUTAGE TIME FOR THE MONTH EXCEEDED 265 HOURS.
TWO FORCED SCRUBBER OUTAGES WERE REPORTED BT THE UTILITY FOR THE
MONTH,  THESE MINOR OUTAGES WERE CAUSED BY PLUGGING IN THE
VENTURI SPRAY HEADERS AND AN I.D. FAN MALFUNCTION*  TOTAL FORCED
OUTAGE TIME AMOUNTED TO 36.8* HOURS.


SCRUBBER OUTAGE fIME WAS REQUIRED FOR INSTALLATION OF A NEW CAR-
BONATE FEED LINE*  IN ADDITION, A MINOR SCRUBBER TRIP WAS CAUSED
BY PLUGGING IN THE SCRUBBER EFFLUENT SUCTION LINE.
                                                               156
                                                                                                  PEOCO ENVIRONMENTAL

-------
                                                         REID GARDNER 1 (CONTINUED)
                  BOILER
          TOTAL  OPERATION
PERIOD     HR.      HR.

NOV. 76    720    631*5

AVAILABILITY - 87*

RELIABILITY = 8t*

OPERABILITY = SIX

UTILIZATION = 71*

DEC. 76    7«»*»     677.H

AVAILABILITY = 93*

RELIABILITY = 92*

OPERABILITY = 88*

UTILIZATION = SOX
AVAILABILITY
    HR.

    623
  HR.
CALLLO
UPON TO
OPERATE

  605
OPERATION
   HR.

   SOS
    690
  652.5
   599
                         COMMENTS

ONE FORCED SCRUBBER OUTAGE OCCURRED DURING THE REPORT PERIOD

BECAUSE OF A SCREW CONVEYOR FAILURE, RESULTING IN AN

INABILITY TO MIX THE CHEMICAL ABSORBENT.
TWO FORCED SCRUBBER OUTAGES OCCURRED DURING DECEMBER BECAUSE

OF CHEMICAL DEPLETION AND A PLUGGED SENSING LINE.
                                                               157
                                                                     PEDCO ENVIRONMENTAL

-------
                                                         REID GARDNER 2
PERIOD

FEB. 75

MAR. 75

APR. 75

MAY  75

JUM. 75
        BOILER
TOTAL  OPERATION

-------
                  BOILER
          TOTAL  OPERATION
PERIOD    (HR.)    (HR.)

OPERABILITY = 66*

UTILIZATION = 62*

FEB. 76    696       675

AVAILABILITY = 6*»*

RELIABILITY = 66*

OPERABILITY = 86*

UTILIZATION = 83*

MAR. 76     7t
-------
                                                         REID GARDNER 2 (CONTINUED)
                  BOILER
          TOTAL  OPERATION
PERIOD    (HR.)    IHR.)

JUU. 76    74*      516

AVAILABILITY = 91S

RELIABILITY = 96*

OPERABILITY = 61*

UTILIZATION = 57*

AUG. 76    7ft       709

AVAILABILITY = 95*

RELIABILITY = 9
-------
                                                         REID GARDNER 2 {CONTINUED)
                  BOILER
          TOTAL  OPERATION
           HR.      HR.

NOV. 76     720      621

AVAILABILITY = 52*

RELIABILITY = SIX

OPERABILITY = 58X

UTILIZATION s SOX

DEC. 76     744      275

AVAILABILITY = OX

RELIABILITY s OX

OPERABILITY = OX

UTILIZATION s OX
                HK.
            CALLEOO
AVAILABILITY  UPON TO
    HR.       OPERATE
                709
OPERATION
   HR.

   363
DURING A BOILER OUTAGE TO REPAIR A CONDENSER TUBE LEAK AND

BOTTOM ASH NOZZLE, THE SCRUBBER'S GUILLOTINE DAMPERS WERE BADLY

DAMAGED, AND THE SCRUBBER REMAINED OUT OF SERVICE DURING THE

MONTH OF DECEMBER.
                                                               161
                                                                     PEDCO ENVIRONMENTAL

-------
                                                             REID GARDNER 3
                  BOILER
          TOTAL  OPERATION
PERIOD    (HR.)    (HR.I
JUL* 76    7**      692
AVAILABILITY = 
-------
                                                          REID GARDNER 3  (CONTINUED)
                  BOILER
          TOTAL  OPERATION   AVAILABILITY
PERIOD     HR.      HR.

NOV. 76    720      264

AVAILABILITY = 28X

RELIABILITY = 29*

OPCRABILITY = 80X

UTILIZATION = 29%

DEC. 76    7«»»»      7«»«»

AVAILABILITY = 99X

.RELIABILITY = 99X

OPERABLIITY = 97S

UTILIZATION = 97X
HR.

205
  HR.

CALLED
UPON TO

OPERATE

  727
737
  728
OPERATION
   HR.
   212
   721
                         COMMENTS
THE SCRUBBER SYSTEM WAS NOT IN OPERATION THE FIRST HALF OF
NOVEMBER DUE TO REPAIRS OF LEAKS IN THE VENTURI SCRUBBER BOX.
THE SYSTEM WAS RESTARTED NOV. 19, AND EXPERIENCED ONE FURTHER
FORCED OUTAGE, BECAUSE OF A SCREW CONVEYOR MALFUNCTION, PRE-
VENTING CHEMICAL MIXING.
DURING THE MONTH, ONE MINOR SCRUBBER OUTAGE, OCCURRED, BECAUSE OF
REPAIRS TO THE I.D. FAN EXPANSION JOINT.
                                                                163
                                                                 PEDCO ENVIRONMENTAL

-------
                  TABLE 3
PERFORMANCE DESCRIPTION FOR OPERATIONAL F60 SYSTEMS  12/76
 IDENTIFICATION NO.

 UTILITY NAME

 UNIT NAME

 UNIT LOCATION

 UNIT RATING

 FUEL CHARACTERISTICS

 FGD VENDOR

 PROCESS

 NEW OR RETROFIT

 START UP DATE

 F6D STATUS

 EFFICIENCY.
  PARTICULATES


  S02
  78

 NORTHERN STATES POWER CO.

 SHERBUKNE COUNTY STATION NO.l

 BECKER MINNESOTA

  710 NW

 COAL O.fi PERCENT SULFUR

 COMBUSTION ENGINEERING

 LIMESTONE SCRUBBING

 NEb

  3/76

 OPERATIONAL


 99 PERCENT GUARANTEE


 SO PERCENT GUARANTEE
 WATER MAKE UP
 SLUDGE DISPOSAL
 UNIT COST
 OPERATIONAL
  EXPERIENCE
 OPEN LOOP 1.13 GPM/MW
 UNSTA8ILIZEQ SLUDGE DISPOSED IN LINED POND
$60 MILLION CAPITAL FOR UNITS 1 AND 3,
 REFER TO THE BACKGROUND INFORMATION SECTION IN TABLE s OF THIS REPORT.
 A PRELIMINARY WATEH/A1H SYSTEM CHECKOUT WAS SUCCESSFULLY COMPLETED BY
 THE UTILITY AND INITIAL OPERATIONS COMMENCED ON MARCH 16, 1976. FULL
 COMMERCIAL OPERATION OF THE SYSTEM BEGAN ON MAY 1, 1976. THE SCRUBBING
 SYSTEM FOR THIS UNIT CONSISTS OF 12 MODULES. EACH SCRUBBING MODULE
 INCORPORATES A VENTURI<-KOD SECTION AND A MARBLE BED ABSORBER FOR PAR-
 TICULATE AND SULFUR DIOXIDE REMOVAL. SYSTEM DESIGN CALLS FOR 11 MODULES
 TO BE IN OPERATION FOR FULL LOAD CAPACITY.
                                                            164
                                                                         PEOCO ENVIRONMENTAL

-------
                                                     BACKGROUND INFORMATION



                                                              ON



                                               SHERBURNE COUNTY GENERATING PLANT



     THE SHERBURNE COUNTY GENERATING PLANT OF THE NORTHERN STATES POWER COMPANY IS LOCATED ON THE MISSISSIPPI RIVER IN SHERBURNE



COUNTY. NEAR BECKER. MINNESOTA.  THIS NEW POWER GENERATING PLANT CURRENTLY HAS ONE COAL-FIRED UNIT OPERATIONAL,ONE UNDER CONSTRUC-



TION* AND TWO IN THE EARLY PLANNING STAGES.  UNIT NO. 1 IS RATED AT 710-NW AND FIRES MONTANA COLSTRlP COAL WITH A HEATING VALUE OF



8300 BTU/LBt AND SULFUR AND ASH CONTENTS OF 0.8 AND 9.0 PERCENT, RESPECTIVELY.  IN ORDER TO MEET PARTICULATE AND SULFUR DIOXIDE



EMISSION STANDARDS WHICH ARE MORE STRINGENT THAN NEW SOURCE PERFORMANCE STANDARDS. THE UNIT WAS FITTtO WITH A SCRUBBING SYSTEM FOR



SIMULTANEOUS PARTICULATE AND SULFUR DIOXIDE REMOVAL.



     THE NORTHERN STATES POWER CO., SHERBUHNE NO. 1 SCKUbBER DESIGN IS BASED UPON THE RESULTS OF A PILOT PLANT TEST PROGRAM CON-



DUCTED AT COMBUSTION ENGINEERING'S  (CE) KREISINGER DEVELOPMENT LABORATORY AND A PROTOTYPE SCRUBBER PROGRAM CONDUCTED JOINTLY BY



COMBUSTION ENGINEERING AND NORTHERN STATES POWER AT THE UTILITY'S BLACK DOG STATION.  THE SCRUBBING SYSTEM IS COMPRISED OF A FIRST



STAGE FIXED-ROD VENTURI  SCRUBBER FOR PARTICULATE REMOVAL  AND A MARBLE BED ABSORBER TO COMPLETE PARTICULATE REMOVAL AND ACHIEVE THE



NECESSARY SULFUR  DIOXIDE REMOVAL.  THE  SCRUBBING SYSTEM HAS BEEN GUARANTEED TO REMOVE 99 PERCENT OF THE PARTICULATE MATTER ENTERING



THE  SCRUBBING  SYSTEM.  OR MAINTAIN  AN EMISSION  0.04 GR/DSCF, WHICHEVER OUTLET VALUE IS GREATER.  THE SULFUR DIOXIDE DESIGN REMOVAL



EFFICIENCY  IS  BASED UPON THE REMOVAL OF  50 PERCENT OF THE SULFUR IN THE FUEL  (MAXIMUM FUEL SULFUR CONTENT OF 1.2 PERCENT) OR



MAINTAIN AN  EMISSION OF  200 PPM. WHICHEVER OUTLET VALUE IS GREATER.



     THE GENERAL  SCENARIO  OF THE SHERBURNE NO. 1 SCRUBBING SYSTEM CONSISTS OF 12 SCRUBBING MODULES, 11 OF WHICH ARE REQUIRED FOR



FULL LOAD CAPACITY. EACH  MODULE HAS A RATED FLUE GAS CAPACITY OF 200,000 TO 220,000 ACFM AT 135 F.  AN AGITATED REACTION TANK IS



LOCATED AT  THE BOTTOM  OF EACH  SCRUBBER MODULE.  THE PURPOSE OF THE REACTION TANK IS TO ALLOW COMPLETION OF SULFUR DIOXIDE FORMA-



TION TO SULFITE,  PROVIDE FORCED OXIDATION  OF SULFITE TO SULFATE, AND FACILITATE PRECIPITATION OF CALCIUM SULFATE SOLIDS.  IN



FORCED  OXIDATION, AIR  IS BUBBLED INTO  THE  REACTION TANK,  OXIDIZING SULFITE TO SULFATE.  THE SULFATE FORMED IS PRECIPITATED IN THE



REACTION TANK  BY  ADDITION  OF GYPSUM SEED CRYSTALS.  A BLEED LINE PROVIDES THE NECESSARY SOLIDS REMOVAL TO A 160-FOOT DIAMETER



CLARIFIER.   HERE  THE WASTE SOLIDS  (FLY ASH, CALCIUM CARBONATE., AND CALCIUM SULFATE) SETTLE OUT AND THE CLARIFIED WATER IS RETURNED



TO  THE  PROCESS.



     THE CLEANED  FLUE  GAS  THEN PASSES  THROUGH  A DOUBLE ROW, TWO-PASS CHEVRON MIST ELIMINATOR.  REHEAT ( T = HO ) IS ADDED TO THE



GAS  STREAM  TO  PROVIDE  PROTECTION TO THE DOWNSTREAM DUCTWORK, I.D. FAN, AND PLUME CONTROL BEFORE FINAL DISCHARGE TO THE ATMOSPHERE.



THE  CLARIFIER  UNDERFLOW  IS PUMPED  TO AN 16-INCH CLAY-LINED SETTLING POND WHICH IS H5-FEET DEEP AND 62 ACRES IN AREA.  THE WATER IS






                                                               165                                PEDCO ENVIRONMENTAL

-------
SHERBURNE COUNTY (CONTINUEDI



RECYCLED FROM THE POND BACK TO THE PROCESS.  A GENERAL FLOW DIAGRAM OF THE SHERBURNE SCRUBBER ARRANGEMENT IS PROVIDED IN FIGURE



16 OF APPENDIX C.



     INITIAL OPERATION OF THE SYSTEM COMMENCED MARCH 16, 197&.  FULL COMMERCIAL OPERATION COMMENCED MAY it 1976.  PROBLEMS ENCOUN-



TERED DURING INITIAL STARTUP OPERATIONS HAVE INCLUDED THE USUAL MECHANICAL PROBLEMS ASSOCIATED WITH A NEW SYSTEM AND SOME PLUGGING



IN THE SCKUBBER INTERVALS.  SPECIFICALLY,  PROBLEMS HAVE BEEN ENCOUNTERED IN THE SPRAY SYSTEM, REQUIRING THE DESIGN OF THE NOZZLES



TO BE CHANGED FROM PLASTIC AND RUBBER COMPONENTS TO CERAMIC SPINNER-VANE COMPONENTS.  ALSO, SOME PLUGGING PROBLEMS HAVE BEEN,



ENCOUNTERED IN THE SPRAY HEADERS,  PRIMARY  CONTACTOR, AND MARBLE BED. THIS HAS STEMMED LARGELY FROM THE MALFUNCTION OF. THE STRAINER



SYSTEM BECAUSE OF POOR NOZZLE CONFIGURATIONS.  NSP IS CURRENTLY MAKING MODIFICATIONS IN THIS AREA.
                                                               166                                PEDCO ENVIRONMENTAL

-------
                                                               SHERBURNE NO
              BOILER OPERATION TIME AND MODULE OPERABILITY
        BOILER
PERIOD   HR.

MAR. 76

APR. 76
MAY  76

JUN. 76
101  102  103  104  105  106  107  106  109  110  111  112
JUL. 76

AUG. 76
                  COMMENTS

A PRELIMINARY SYSTEM CHECKOUT BY PASSING WATER AND

AIR THROUGH THE SYSTEM WAS SUCCESSFULLY COMPLETED.

THE SYSTEM WAS INITIALLY PLACED IN SERVICE MARCH

16. 1976.  FIRST COMMERCIAL OPERATION COMMENCED

MAY 1. 1976.  THIS IS AN INTERMEDIATE LOAD UNIT,

OPERATING AT OR NEAR FULL CAPACITY DURING THE DAY

AND 35 PERCENT CAPACITY AT NIGHT.  MODIFICATIONS

ARE PROCEEDING ON THE SPRAY SYSTEM, SPRAY NOZZLES,

AND STRAINER SYSTEM.

DEVELOPMENTAL WORK IS CONTINUING ON THIS SCRUBBING

SYSTEM.  SINCE JULY 1, THE NO. 1 UNIT HAS BEEN

GENERATING 95 TO 98 PERCENT THE NUMBER OF MW-HOURS

THAT HAVE BEEN REQUIRED.  THE NO. 1 UNIT IS AN

INTERMEDIATE LOAD UNIT WHICH OPERATES AT FULL

CAPACITY 15-16 HOURS/DAY AND ONE-THIRD CAPACITY

THE REMAINDER.  PLUGGING IN THE SLURRY NOZZLES IS

STILL A PROBLEM.  A QUARTER-INCH PARTICLE IN

THE FEED SOLUTION WILL PLUG UP THE FEED NOZZLES.

NSP is NOW PLANNING TO MODIFY THE DUPLEX STRAINER

SYSTEM TO ALLEVIATE THIS PROBLEM.  IN ADDITION,

THE DEPOSITION OF SOFT SOLIDS IS STILL CONTINUING

IN THE DEMISTERS AND REHEATERS.  HARD SCALE

GYPSUM FORMATION ON THE VESSEL WALLS HAS LEVELED

OFF.  A CREW OF 70 PEOPLE IS REQUIRED TO MAINTAIN
                                                               167
                                                                                  PEDCO ENVIRONMENTAL

-------
                                                    SHERBURNE NO. 1 (CONTINUED)
              BOILER OPERATION TIME AND NODULE OPERABILXTY
        BOILER
PERIOD   HR.    101  102  10}  10H  105  106  107  106  109  110  111  112
SEP. 76    566     87   90   93   76   76
TOTAL SYSTEM AVAILABILITY = 95 PERCENT
TOTAL SYSTEM OPERABILITY = 100.0 PERCENT
OCT. 76    606     97   8H   96   96   93
TOTAL SYSTEM AVAILABILITY = 93 PERCENT
TOTAL SYSTEM OPERABILITY s 100 PERCENT
79   85
79
85   80   92   96
30   7H   76   91   81  100
                    67
                  COMMENTS
SCRUBBER OPERATIONS.  THE PREVENTIVE MAINTENANCE
AND CLEANING PROCEDURES NOW EMPLOYED FOR THE
SCRUBBING SYSTEM CALLS FOR 3 TO 4 MODULES TO BE
TAKEN OUT OF SERVICE EACH NIGHT.  THEREFORE*
EACH MODULE IS CLEANED OuT ONCE EVERY THREE DAYS.
THE TOTAL SYSTEM AVAILABILITY INDEX IS DEFINED AS
THE AMOUNT OF TIME 11 MODULES ARE AVAILABLE TO THE
UNIT, THUS ALLOWING FULL LOAD CAPACITY CAPABILITY.
TOTAL SYSTEM OPERABILITY HAS TO BE 100 PERCENT
SINCE THE SCRUBBERS CANNOT BE BYPASSES TO OPERATE
THE BOILER. NSP IS NOW IN THE PROCESS OF MODIFYING
THE SYSTEM'S STRAINER DESIGN.  THE DUPLEX UNITS
ARE GOING TO BE RETIRED AND REPLACED WITH IN-THE-
TANK SCREENS AND SOOT BLOWERS, BOTH LOCATED AT
THE SUCTION SIDE OF THE RECYCLE PUMP.  CARBON
STEEL FIN TUBE REHEAT BUNDLES ARE ALSO AN AREA OF
CONCERN.  MULTIPLE FAILURES IN FOUR UNITS HAVE
BEEN EXPERIENCED.
                                                               168
                                                      PEOCO ENVIRONMENTAL

-------
                                                    SHERBURNE NO.l (CONTINUED)

              BOILER OPERATION TIME AND MODULE. AVAILABILITY
        BOILER
PERIOD     HR.    101  102  103  104  105  106  107  108  109  110  111  112
NOV. 76    720     83   80   87   79   92

TOTAL SYSTEM AVAILABILITY = 93 PERCENT

TOTAL SYSTEM OPERABILITY = 100 PERCENT
DEC. 76    722     88   6H   87   60   71

TOTAL SYSTEM AVAILABILITY s 95 PERCENT

TOTAL SYSTEM OPERABILITY = 100 PERCENT
80   93   89   69   78   73   93
97   91
95
91   88   73   75
                  COMMENTS

THE MODIFICATION OF THE DUPLEX STRAINER SYSTEM

IS ONGOING, CURRENTLY APPROXIMATELY ONE-THIRD

COMPLETED ON THE NO. 1 UNIT.  THE UTILITY IS

NOW CONDUCTING A FULL-LOAD EVALUATION STUOYt

ANALYZING SYSTEM OPERATION ON 10 MODULES VS.

THE DESIGNED 11 MODULES.  THE UNIT IS CURRENTLY

HAVING DIFFICULTY COMPLYING WITH THE 20 PERCENT

OPACITY REGUALTION, DUE TO THE EXTREMELY FINE

FLY ASH BEING EMITTED (70 PERCENT LESS THAN

ONE MICRON.)
                                                               169
                                                      PEDCO ENVIRONMENTAL

-------
                  TABLE 3
PERFORMANCE DESCRIPTION FOR OPERATIONAL F6D SYSTEMS  12/76
 IDENTIFICATION NO.

 UTILITY NAME

 UNIT NAME

 UNIT LOCATION

 UNIT RATING

 FUEL CHARACTERISTICS

 FGD VENDOR

 PROCESS

 NEW OK RETROFIT

 START UP DATE

 FGQ STATUS

 EFFICIENCY,
  PARTICULATES
  84

 PENNSYLVANIA  POWER  CO.

 BRUCE  MANSFIELD NO.  1

 SHIPPINGPORT  PENNSYLVANIA

  635 MM

 COAL t.7  PERCENT SULFUR

 CHEMICO

 LIME SCRUBBING

 NEW

  H/76

 OPERATIONAL


 99.8 PERCENT
  S02
 92 PERCENT GUARANTEE
 WATER MAKE UP
 SLUUGE DISPOSAL
 CLOSED LOOP
  STABILIZED SLUDGE DISPOSED IN  UNLINED POND
 UNIT COST
 OPERATIONAL
  EXPERIENCE
S133/KW CAPITAL * 2.7 MILLS/  KWH ANNUALIZED
 REFER TO THE BACKGROUND INFORMATION SECTION IN TABLE 3 OF THIS REPORT.
 THIS EMISSION CONTROL SYSTEM IS CAPABLE OF REMOVING FLYASH AND S02 FROM
 3.35 MM ACFrt OF FLUE GAS VIA MET LIME SCRUBBING. THE INITIAL SHAKEDOWN
 AND DEBUGGING PHASE OF OPERATION BEGAN FOR PART OF THE SYSTEM IN DECEMBER
 1975. FULL COMMERCIAL OPERATION COMMENCED IN APKIL 1976. TO DATE, ALL 6
 OF  THE SCRUBBING TRAINS HAVE BEEN SUCCESSFULLY PUT INTO OPERATION.
 THE AVAILABILITY INDEX VALUE FOR THE ENTIRE SCRUBBING SYSTEM HAS
 BEEN IN THE MID 90 PERCENT RANGE SINCE COMMERCIAL START-UP.
                                                            170
                                                                         PEOCO ENVIRONMENTAL

-------
                                                     BACKGROUND INFORMATION



                                                               ON



                                                   BRUCE MANSFIELD UNIT NO. 1



     THE BRUCE MANSFIELD PLANT IS A 2700-MH, THREE-UNIT, COAL-FIRED FACILITY LOCATED ON THE OHIO RIVER IN THE BOROUGH OF SHIPPING



PORT* PENNSYLVANIA. THIS NEW FACILITY IS BEING BUILT BY PENNSYLVANIA POWER CO., WHICH IS ACTING ON ITS OWN BEHALF AND AS AGENT FOR



THE OTHER PARTICIPATING COMPANIES* THE CLEVELAND ELECTRIC ILLUMINATING CO., DUQUESNE LIGHT CO., OHIO EDISON CO., AND TOLEDO EDISON




CO.



     BRUCE MANSFIELD NO. 1 IS A COAL-FIRED, ONCE-THROUGH, SUPERCRITICAL STEAM GENERATOR WHICH FIRES 333 TONS/HR OF COAL GENERATING



APPROXIMATELY 6.5 MM LB/HR OF STEAM AT 3*765 PSIG, 1005 F/1005 F.  THE EMISSION CONTROL EQUIPMENT REQUIRED FOR THIS UNIT IS



DESIGNED TO MEET STATE EMISSION REGULATIONS OF 0.6 LBS SULFUR DIOXIDE/MM BTU OF HEAT INPUT AND 0.0175 GR/SCF OF PARTICULATE WHEN



BURNING 11,900 BTU/L8 COAL HAVING AVERAGE ASH AND SULFUR CONTENTS OF 12.5  AND t.7 PERCENT. RESPECTIVELY.



     IN LATE 1970. AN INTENSIVE INVESTIGATION OF MORE THAN  30 POTENTIAL DESULFURIZATION SYSTEMS WAS INITIATED*  THE SYSTEM ULTI-



MATELY CHOSEN FOR THE REMOVAL OF FLY  ASH AND SULFUR DIOXIDE WAS THE VENTURI WET-SCRUBBING SYSTEM* MANUFACTURED BY CHEMICO AIR



POLLUTION CONTROL CO., UTILIZING THE  DRAVO  CORPORATION'S THIOSORBIC LIME AS THE SCRUB8ING-ABSORBENT.



     THE DESIGN  FEATURES  OF  THE SCRUBBING  SYSTEM DICTATES EACH SCRUBBING TRAIN CONSIST OF A SCRUBBING VESSEL (VARIABLE-THROAT



VENTURI), A  9000-HR  I.Q.  FAN, AND  AN  ABSORBER VESSEL  (FIXED-THROAT VENTURI). THERE ARE SIX SCRUBBER TRAINS PER UNIT, FIVE OF WHICH



ARE  REQUIRED TO  HANDLE  THE FLUE GAS FLOW FROM THE BOILER AT FULL LOAD  (3.35 MM ACFM AT 285 F).  THE SCRUBBER/ABSORBER TRAINS ARE



ARRANGED  IN  TWO  GROUPS  OF THREE.   THE TREATED FLUE GAS, WHICH HAS PASSED THROUGH THE SCRUBBING SYSTEM, IS DUCTED THROUGH A COMMON



REHEAT  CHAMBER ANU  THEN EXHAUSTED  UP  THE 950-FT. STACK.



     THE  ADJUSTABLE  VENTURI  THROAT SCRUBBING MODULE REMOVES NEARLY ALL OF  THE FLY ASH CONTAINED ZN THE FLUE GAS.  THE ABSORBER



MODULE,  WHICH  IS A  FIXED-THROAT VENTURI, REMOVES THE REMAINING FLY ASH.  SULFUR DIOXIDE IS ABSORBED IN BOTH THE SCRUBBER AND



ABSORBER  e»Y  DROPLETS OF LIME SLURRY.  CONTAINING 2 TO 6 PERCENT MAGNESIUM OXIDE,



     THE  SCRUBBER-RECYCLE BLEED IS COMBINED WITH A FLY ASH  SLURRY FROM THE BOILER AND DISCHARGED TO A 200-FOOT-DZAMETER THICKENER.



SLUDGE  FROM  THE  THICKENER IS THEN  PUMPED TO A WASTE DISPOSAL SYSTEM WHERE  IT IS MIXED WITH A STABILIZING AGENT (CALCILOX) AND THEN



PUMPED  APPROXIMATELY 7  MILES TO THE LITTLE  BLUE RUN RAVINE  FOR LAND FILL.



     A  SIMPLIFIED PROCESS FLOW DIAGRAM IS PRESENTED IN FIGURE 17 OF APPENDIX C.
                                                                                                  PEOCO ENVIRONMENTAL

-------
MONTH
                                                            BRUCE MANSFtELD NO. 1
BOILER
   OPERATING HOURS
     FGD MODULES
                                                 COMMENTS
DEC. 75



JAN. 76

FEB. 76

MAR. 76

APR. 76
  506
210
MAY  76     595         209    615

TOTAL SYSTEM AVAILABILITY s. 60*

TOTAL SYSTEM OPERABILITY s 108*

TOTAL SYSTEM RELIABILITY a 100*

TOTAL SYSTEM UTILIZATION = 60*

JUN.76      72Q         711    660

TOTAL SYSTEM AVAILABILITY s 100K

TOTAL SYSTEM OPCRABILITY * 1003

TOTAL SYSTEM RELIABILITY « 100*

TOTAL SYSTEM UTILIZATION e 100*

JUU. 76    672.«        537    S9fl

TOTAL SYSTEM AVAILABILITY s 968

TOTAL SYSTEM OPERABILITY s 100*

TOTAL $YSJC« RELIABILITY * 100*

TOTAL SYSTEM UTILIZATION s 90S
2147
24Q6
2H27
                            1576   2659
                      3430
                2920
                             701
               674
         705
         578
                             606
               637
         662
         661
                                                            INITIAL OPERATION (SHAKEDOWN AND DEBUGGING) FOR PART OF THE

                                                            SYSTEM COMMENCED IN DECEMBER 1975.
THE INSTALLATION BEGAN FULL COMMERCIAL OPERATION IN APRIL.

THE SCRUBBING SYSTEM IS CURRENTLY HANDLING FLUE GAS AT A

TOTAL EQUIVALENT CAPACITY OF 840 TO 850-MU (GROSS).  THE

TOTAL MODULE BY MODULE OPERATION HOURS LOGGED TO-OATE ARE

POSTED IN THE ACCOMPANYING TABLE.

THE LAST SCRUBBING TRAIN WAS PLACED IN SERVICE DURING THE

MONTH.  SERVICE TIME TOTALS FOR ALL 6 SCRUBBER-ABSORBER

TRAINS THROUGH MAY ARE POSTED IN THE ACCOMPANYING TABLE

ALONG WITH THE PERFORMANCE INDEX VALUES.



 THE VALUES IN THE ACCOMPANYING TABLE ARE THE BOILER HOURS

 AND THE MODULAR OPERATING HOURS.
                                                               172
                                                                                        PEOCO ENVIRONMENTAL

-------
                                                           BRUCE MANSFIELD NO.  1 (CONTINUED)

                                  OPERATING HOURS
MONTH     BOILER                    FGD MODULES                                               COMMENTS
                         A      B       C      0       £       F

AUG. 76    705.3        672    620     655    535     500     668

TOTAL SYSTEM AVAILABILITY = 95X

TOTAL SYSTEM OPCRABILITY = 100X

TOTAL SYSTEM RELIABILITY = 100*

TOTAL SYSTEM UTILIZATION = 95X

SEP. 76     720         706   617      693    695     596     H6H

TOTAL SYSTEM AVAILABILITY = 1008

TOTAL SYSTEM OPERABILITY = 100%

TOTAL SYSTEM RELIABILITY = 10OK

TOTAL SYSTEM UTILIZATION = 100X

OCT. 76     739         710    549      631    619     691     691

TOTAL SYSTEM AVAILABILITY = 99X

TOTAL SYSTEM OPERABILITY = 10OX

TOTAL SYSTEM RELIABILITY = 100X

TOTAL SYSTEM UTILIZATION = 99X

NOV. 76      277          270      278    282    113     159     2t6

TOTAL SYSTEM AVAILABILITY = 100X

TOTAL SYSTEM OPERABILITY = 100 X

TOTAL SYSTEM RELIABILITY = 100 X

TOTAL SYSTEM UTILIZATION = 38X

DEC. 76     722         58«»    726     68*    433     622     626

TOTAL SYSTEM AVAILABILITY = 100  X

TOTAL SYSTEM OPERABILITY = 100 X

TOTAL SYSTEM RELIABILITY = 100 X

TOTAL SYSTEM UTILIZATION =97X


                                                               173                                PEOCO ENVIRONMENTAL

-------
                  TABLE 3
PERFORMANCE DESCRIPTION FOR OPERATIONAL FGO SYSTEMS  12/76
 IDENTIFICATION NO.

 UTILITY NAME

 UNIT NAME

 UNIT LOCATION

 UNIT RATING

 FUEL CHARACTERISTICS

 FGD VENDOR

 PROCESS

 NEW OR RETROFIT

 START UP DATE

 FGD STATUS

 EFFICIENCY.
  PARTICULATES
  80

 PHILADELPHIA ELECTRIC CO.

 EBCYSTONE NO 1A

 EDOYSTONE PENNSYLVANIA

  120 MU

 COAL   2.5 PERCENT SULFUR

 UNITED ENGINEERS / PECO

 MAGNESIUM OXIDE SCRUBBING

 RETROFIT

  9/75

 OPERATIONAL


 99.9 PERCENT
  S02
 WATER MAKE UP
 SLUObE DISPOSAL
 UNIT COST
 OPERATIONAL
  EXPERIENCE
 90 PERCENT
 CLOSED LOOP 1.1 GPM/MW
$17 MILLION CAPITAL
 REFER TO THE BACKGROUND INFORMATION SECTION IN TABLE 3 OF THIS REPORT.
 THE &02 SCRUBBING OPERATIONS HAVE BEEN TEMPORARILY DISCONTINUED AT THIS
 STATION BECAUSE THE REGENERATION FACILITY AT THE OLIN CHEMICAL SULFURIC
 ACID PLANT HAS PERMANENTLY CEASED OPERATIONS.  THE UTILITY IS NOW RELO-
 CATING THE REGENERATION FACILITY TO THE ESSEX CHEMICAL PLANT LOCATED
 IN NEWARKi NEW JERSEY, RESUMPTION OF $02 SCRUBBING OPERATIONS js NOW
 SCHEDULED FOR MAY OF 1977.  To DATE. THE MAGNESIUM OXIDE SCRUBBING UNIT
 HAS BEEN IN SERVICE FOR ONLY A SHORT PERIOD OF TIME DURING LATE 1975,
                                                            17*
                                                                         PEOCO ENVIRONMENTAL

-------
                                                     BACKGROUND INFORMATION



                                                              ON



                                                        EDDYSTONE NO. 1



     THE EDDYSTONE STATION OF THE PHILADELPHIA ELECTRIC COMPANY (PECO) IS LOCATED ON THE DELAWARE RIVER IN EODYSTONE,PENNSYLVANIA.



ABOUT 11 MILES SOUTHWEST OF THE CENTER OF PHILADELPHIA.  THE PLANT IS APPROXIMATELY FIVE MILES WEST OF ONE OF THE MAIN RUNWAYS OF




THE PHILADELPHIA INTERNATIONAL AIRPORT.



     THE STATION HAS FOUR GENERATORS WITH A TOTAL NET GENERATING CAPACITY OF 1370 MW.  UNITS 1 AND 2 BURN COAL WITH AN AVERAGE



GROSS HEATING VALUE OF 12.100 BTU/LB AND ASH AND SULFUR CONTENTS OF 12 PERCENT AND 2.3 PERCENT, RESPECTIVELY. STEAM CONDITIONS ARE



5.000 PSI AND 1150 F.  THESE ARE THE HIGHEST UTILITY PLANT OPERATING PRESSURE AND TEMPERATURE CONDITIONS IN THE UNITED STATES.



UNITS 1 AND 2 ARE BASE-LOAD UMTS.  UNITS 3 AND 
-------
EODYSTONE (CONTINUED)
     THE MAGNESIUM OXIDE REGENERATION FACILITY HAS BEEN OPERATED TO PROCESS ALL MAGNESIUM SULFITE MATERIAL SENT TO IT FROM EDDY-
STONE.  THIS OPERATION WAS USUALLY ON A BATCH BASIS DUE TO THE UPS AND DOWNS AT THE EDDYSTONE SCRUBBER.
     THE SULFUR DIOXIDE SCRUBBING SYSTEM WAS TEMPORARILY SHUT DOWN DECEMBER 31t 1975i  BECAUSE THE ACID PLANT REGENERATION FACILITY
AT THE OLIN CHEMICAL SULFURIC ACID PLANT IN PAULSBORO, NEW JERSEY PERMANENTLY CEASED OPERATIONS. THE UTILITY IS NOW IN THE PROCESS
OF RELOCATING THE REGENERATION FACILITY-TO THE ESSEX CHEMICAL PLANT LOCATED IN NEWARKt NEW JERSEY. THE RELOCATION OF THIS FACILITY
WILL PROBABLY PROLONG THE SULFUR DIOXIDE DEVELOPMENTAL SCHEDULE BY APPROXIMATELY ONE YEAR.  THE WET PARTlCULATE SCRUBBERS ARE.
CONTINUING TO OPERATE AT THE EOOYSTONE PLANT.
     THE PARTlCULATE AND SULFUR DIOXIDE REMOVAL SYSTEM INSTALLED ON THE EODYSTONE NO.  1 UNIT IS THE FIRST PHASE OF A TWO-PHASE
PROJECT.  FOLLOWING SUCCESSFUL DEVELOPMENT OF THIS SYSTEM WITH MORE CONTINUOUS OPERATION, IT WILL BE  INCORPORATED INTO THE DESIGN
FOR THE COMPLETE SULFUR DIOXIDE REMOVAL ON EODYSTONE NO. 2 AND ONE OF THE TWO EXISTING UNITS AT THE CROMBY STATION.
     ADDITIONAL INFORMATION AND DATA CONCERNING THE OPERATION OF THE PARTlCULATE AND SULFUR DIOXIDE SCRUBBERS INSTALLED AT TH.IS
PLANT ARE PROVIDED IN THE PERFORMANCE TABLE.
                                                               176                                PEOCO ENVIRONMENTAL

-------
                                                     F60 SYSTEM PERFORMANCE
                                                         EODYSTONE NO. 1
                                                             COMMENTS
NOV. 7H   THE SCRUBBING SYSTEM AT THIS PLANT CONSISTS OF THREE PARALLEL SCRUBBING TRAINS INCORPORATING 3 WET PARTICULATE SCRUBBERS
DEC. 7<»   AND ONE S02 ABSORBER MODULE.  THERE WAS A BKIEF OPERATING PERIOD ON THE PARTICULATE SCRUBBERS FROM MID-NOVEMBER 197«t TO
JAN. 75   MARCH 1975.  PROBLEMS ENCOUNTERED CENTERED AROUND THE SCRUBBER BOOSTER FANS AND THE FLUE GAS AND LIQUID CONDITIONS.
FEB. 75   THE B-SIDE BOOSTER FAN DEVELOPED HIGH SHAFT VIBRATION WHEN STARTED FOR THE FIRST TIME.  THIS PROBLEM WAS DESIGN-RELATEOt
MAR. 75   INVOLVING AN EXCESSIVE CLEARANCE AREA BETWEEN THE SHAFT AND THE WHEEL HUB.  ALSO, EXTENSIVE CORROSION DEVELOPED IN THE
APR. 75   C-SIDE PARTICULATE SCRUBBER INTERNALS.  THIS WAS CAUSED BY LOW SCRUBBING SOLUTION PH LEVELS AND CHLORIDE LEVELS AS HIGH
MAY  75   AS 2000 PPM.  THESE CONDITIONS COUPLED WITH THE THERMAL SHOCK OF A HOT START PROCEDURE CAUSED THE CORROSION.  THIS
JUN. 75   PROBLEM WAS AMELIORATED BY CAUSTIC ADDITION* HIGHER SLOWDOWN AND EMPLOYING A COLO START PROCEDURE.  AT APPROXIMATELY
          THIS TIME, A CHECKOUT OF SQ2 SYSTEM WAS CONDUCTED.  BLISTERING AND PEELING OF THE POLYURETHANE COATINGS WERE DETECTED
          AND CORRECTED BY RECOATING WITH FLAKE GLASS.
JUL. 75   THE C-SIDE: PARTICULATE SCRUBBER RESTARTED  ON JULY 23. 1975,  THE TWO REMAINING TRAINS. B-SIDE AND A-SIOE, WERE PUT INTO
AUG. 75   OPERATION ON AUGUST  15 AND OCTOBER 2, RESPECTIVELY.  THE S02 ABSORBER MODULE IN THE C-SIDE SCRUBBING TRAIN WAS INITIALLY
SEP. 75   PLACED  IN SERVICE  OCTOBER 2. 1975.  THE OLIN CHEMICAL MGO REGENERATION FACILITY FIRST PROCESSED MAGNESIUM SULFITE FROM
OCT. 75   THE EDDYSTONE SCRUBBER ON OCTOBER 28, 1975.  THE C-SIDE PARTICULATE SCRUBBER OPERATED A TOTAL OF 2831 HOURS THROUGH
NOV. 75   JANUARY 31.  1976,  FOR  AN AVAILABILITY OF 70 PERCENT.  THHE B-SIDE TRAIN HAS OPERATED A TOTAL OF 1933 HOURS THROUGH
DEC. 75   JANUARY 31.  1976 FOR AN AVAILABILITY OF 55 PERCENT.  THE A-SIDE TRAIN OPERATED A TOTAL OF 626 HOURS THROUGH JANUARY 31.
JAN. 76   1976, FOR  AN AVAILABILITY OF 2H PERCENT.   THE C-SIDE S02 ABSORBER WAS IN SERVICE A TOTAL OF 556 HOURS THROUGH DECEMBER
          31, 1975,  WITH  AN  AVAILABILITY OF 33 PERCENT SINCE STARTUP. PROBLEMS ENCOUNTERED IN THE OPERATION OF THE THREE SCRUBBING
          TRAINS  INCLUDED*   UNDER-DESIGNED RECIRCULATION PUMPS, MALFUNCTION OF THE FLUE GAS BY-PASS DAMPER DRIVE UNITS AND
          FAILURE OF  THE  DOUBLE-BRICK REFRACTORY LINING IN THE REHEAT COMBUSTION CHAMBER.
FEB. 76   OPERATION  OF THE SQ2 SCRUBBING SYSTEM AT EDDYSTONE WAS TEMPORARILY HALTED BECAUSE THE ACID PLANT REGENERATION FACILITY
MAR. 76   AT THE  OLIN  CHEMICAL SULFURIC ACID PLANT IN PAULSBORO, NEW JERSEY PERMANENTLY CEASED OPERATIONS.  THE UTILITY IS NOW
APR. 76   INVESTIGATING ALTERNATIVE REGENERATION SITES.  A MINIMUM PERIOD OF SIX MONTHS WILL BE REQUIRED FOR RELOCATION ONCE A
                                                               177                                PEOCO ENVIRONMENTAL

-------
                                              FGO SYSTEM PERFORMANCE (CONTINUED)



                                                        EODYSTONE NO.  1



                                                            COMMENTS



HAY  76   CHOICE Is MADE.   THE  UTILITY  ANNOUNCED PLANS FOR RELOCATION  OF THE REGENERATION FACILITY  AT  THE  ESSEX  CHEMICAL PLANT  IN



          NEWARK.  NEW JERSEY.



JUN. 76   RESUMPTION OF S02 SCRUBBING OPERATIONS IS PRESENTLY SCHEDULED FOR DECEMBER 1976.  THE RELOCATION OF  THE REGENERATION



JUL. 76   FACILITY IS NOW  IN PROGRESS.   THE PARTlCULATE SCRUBBERS ARE  OPERATIONAL.   THE C-SIDE BOOSTER FAN HAS DEVELOPED A



AUG. 76   MATERIALS FAILURE BETWEEN THE HUB AND SHAFT (IDENTICAL TO THE B-SIDE UNIT MENTIONED ABOVE).



SEP. 76   ALL THREE BOOSTER FANS HAVE NOW DEVELOPED THE MATERIALS FAILURE BETWEEN THE HUB AND SHAFT (AS IDENTIFIED IN THE ABOVE



OCT. 76   FOR THE B-SIDE UNIT).  THESE  UNITS HAVE BEEN RETURNED TO THE MANUFACTURER FOR MODIFICATIONS  AND  REPAIRS.  CURRENTLY,  ONE



          OF THE PARTICULATE SCRUBBERS  is IN THE FLUE GAS STREAM.  TO  DATE. ALL THREE OF THE WET PANICULATE SCRUBBERS HAVE NOT



          SEEN ANY APPRECIABLE  SIMULTANEOUS SERVICE TIME.



NOV. 76   MGO SCRUBBING OPERATIONS ARE  NOW SCHEDULED TO RESTART IN HAY 1977.  REGENERATION FACILITY RELOCATION IS BEING COM-



DEC. 76   PLETED, AND MODIFICATIONS TO  THE ID BOOSTER FANS CURRENTLY BEING EFFECTED CONSIST OF CONVERSION  FROM A SHRINK FIT



          TO A SLIP FIT.  THESE MODIFICATIONS ARE EXPECTED TO ELIMINATE RECURRING VIBRATION PROBLEMS.
                                                               176                                PEDCO ENVIRONMENTAL

-------
                  TABLE 3
PERFORMANCE DESCRIPTION FOR OPERATIONAL F60 SYSTEMS  12/76
 IDENTIFICATION NO.

 UTILITY NAME
 UNIT NAME
 UNIT LOCATION
 UNIT RATING
 93

PUBLIC SERVICE CO OF COLORADO

VAL.10NT NO. 5

VALNONT COLORADO

  SO MU
  FUEL CHARACTERISTICS  COAL  0.72 PERCENT SULFUR
  FGD VENDOR

  PROCESS

  NEW OR RETROFIT

  START UP DATE

  FGD STATUS

  EFFICIENCY*
   PARTICULATES


   S02
 UOP  /  PUB  SERVICE  OF  COLORADO

 LIMESTONE  SCRUBBING

 RETROFIT

 10/7H

 OPERATIONAL


 95 PERCENT


 65 PERCENT
   WATER MAKE UP
   SLUDGE DISPOSAL
 CLOSED LOOP
 UNSTABILIZED  SLUDGE DISPOSED IN LINED POND
   UNIT COST
   OPERATIONAL
    EXPERIENCE
  REFER  TO  BACKGROUND  INFORMATION SECTION IN TABLE 3 OF THIS REPORT. THIS
  SYSTEM HAS  BEEN  OPERATIONAL SINCE NOVEMBER 197*. THE FGt SYSTEM CURRENTLY
  OPERATIONAL AT THIS  STATION IS AN EXPERIMENTAL UNIT. ORIGINALLY DESIGNED
  BY  UNIVERSAL OIL PRODUCTS FOR PARTICULATE REMOVAL ONLY. ONE OF THE THO
  PARALLEL  SCRUBBING MODULES WAS CONVERTED TO LIMESTONE SCRUBBING FOR
  EXPERIMENTAL PURPOSES ONLY.
                                                              179
                                                                         PCOCO ENVIRONMENTAL

-------
                                                     BACKGROUND INFORMATION
                                                                ON
                                                          VALMONT NO.  5
     THE VALMONT POWER STATION OF THE PUBLIC SERVICE COMPANY OF COLORADO IS LOCATED IN VALMONT, COLORADO,  APPROXIMATELY 20 MILES
NORTH OF DENVER.  VALMONT NO.  & IS A COAL-FIRED UNIT BURNS THAT FIRES  GAS A FEW MONTHS DURING THE YEAR.   THE COAL GENERALLY
EMPLOYED FOR THIS UNIT IS WYOMING ROSEBUD, WHICH HAS AN AVERAGE GROSS  HEATING VALUE OF 10.760 BUT/LB WITH ASH CONTENT IN THE & TO
7 PERCENT RANGE ANQ SULFUR CONTENT LESS THAN 1 PERCENT.
     THE FGD SYSTEM BEING TESTED AT THIS STATION is AN EXPERIMENTAL UNIT ORIGINALLY DESIGNED BY UNIVERSAL OIL PRODUCTS FOR PARTIC-
ULATE REMOVAL ONLY.  THIS TCA UNIT CONSISTS OF TWO PARALLEL MODULES WITH A COMBINED CAPABILITY OF TREATING APPROXIMATELY 50
PERCENT OF THE TOTAL FLUE GAS LOAD OR THE EQUIVALENT OF APPROXIMATELY  100 MW GENERATING CAPACITY (50 MW  PER MODULE).  THIS SYSTEM
WAS COMPLETED AND OPERATIONAL IN 1971 AND RAN UNTIL OCTOBER 1971.  PARTICIPATE REMOVAL EFFICIENCY WAS MEASURED AT 95 PERCENT,
SULFUR DIOXIDE REMOVAL EFFICIENCY WAS <*S PERCENT, AND AVAILABILITY WAS APPROXIMATELY 70 PERCENT.  FREQUENT SCRUBBER OUTAGES WERE
CAUSED PRIMARILY BY SUPERSATURATED CALCIUM SULFATE IN THE SCRUBBING LIQUOR.  TO MINIMIZE CLEANOUTS AND RECTIFY SCALING PROBLEMS*
A PH CONTROL PROGRAM WAS IMPLEMENTED FOR ONE OF THE SCRUBBING MODULES  WITH ADDITION OF LIMESTONE TO THE  SCRUBBING LIQUOR. THIS
MODIFICATION WAS EXPECTED TO MINIMIZE SCALING, DECREASE SCRUBBER OUTAGES FOR CLEANOUTS* AND INCREASE AVAILABILITY.  THE EXPECTED
RESULTS DID MOT MATERIALIZE.  SCALE BUILDUP CONTINUED AND AVAILABILITY DECREASED.  TESTS DURING THE PH CONTROL PROGRAM SHOWED
PARTICULATE REMOVAL EFFICIENCY AT 95 PERCENT*  SULFUK DIOXIDE REMOVAL  EFFICIENCY INCREASED TO 85 PERCENT* AND AVAILABILITY DROPPED
TO 70 PERCENT.  THE UNSTABILIZED SLUDGE GENERATED DURING THIS OPERATION WAS PUMPED TO A LINED POND.  THE OPERATIONAL DATA GENER-
ATED FROM THE LIMESTONE MODIFICATION PROGRAM ARC PRELIMINARY* BASED UPON A 4.5 MONTH TESTING PROGRAM.
                                                               160                                PEOCO ENVIRONMENTAL

-------
                                                                VALMONT NO. S
MONTH

SEP. 75

OCT. 75

NOV. 75

DEC. 75



JAN. 76

FEB. 76



MAR. 76

APR. 76

MAY  76

JUN. 76

JUL. 76

AUG. 76
SEP.  76

OCT.  76
    OPERATING HOURS
BOILER     FGO SYSTEM
  FGD SYSTEM
OPEKABILITY (X)
NOV.  76

DEC.  76
                         COMMENTS

THIS FACILITY HAS BEEN INACTIVE SINCE SEPTEMBER 1«  1975. BECAUSE OF A

TURBINE GENERATOR FAILURE.  THE UNIT IS SCHEDULED TO GO ON LINE AGAIN

IN DECEMBER 1975.  THIS UNIT IS STILL INACTIVE BECAUSE OF A BOILER

OVERHAUL. THE SCRUBBER/ABSORBER TRAIN IS AVAILABLE AND WILL BE COUPLED

INTO THE SYSTEM WHEN THE BOILER GOES BACK ON-LINE.

THE BOILER OVERHAUL HAS BEEN COMPLETED.  THE UNIT IS AVAILABLE IN THE

PARTICULATE REMOVAL MODE ONLY*  THE UTILITY IS SUSPENDING RESUMPTION

OF THE LIMESTONE MODIFICATION OPERATION FOR AN INDEFINITE PERIOD.

THE EXPERIMENTAL LIMESTONE SCRUBBING PROGRAM WAS INACTIVE DURING THE

REPORT PERIOD.  RESUMPTION OF THE PROGRAM IS CONSIDERED INDEFINITE AT

THE PRESENT TIME.THE EXPERIMENTAL LIMESTONE SCRUBBING PROGRAM REMAINED

INACTIVE DURING THE REPORT PERIOD.  PRESENT PLANS CALL FOR THE RESUMP-

TION OF THIS PROGRAM SOMETIME IN THE FALL OF 1976.  THE TCA UNIT IS

NOW OPERATIONAL IN THE PARTICULATE REMOVAL MODE.  THE NO. 5 UNIT FIRES

A COMBINATION OF COAL AND NATURAL GAS MEETING CURRENT STATE AIR

EMISSION STANDARDS.

NO CHANGE IN STATUS.  THE RESUMPTION OF THE EXPERIMENTAL LIMESTONE

ADDITIONAL AND S02 REMOVAL PROGRAM IS STILL INDEFINITE.  THE TCA

MODULES ARE CONTINUING TO OPERATE IN THE PARTICULATE REMOVAL MODE.

CARRYOVER INTO THE RECIRCULATION SYSTEM IS STILL A PROBLEM AREA.

THE LOW PH SCRUBBER ENVIRONMENT HAS CAUSED A MATERIALS PROBLEM,

NECESSITATING REPLACEMENT OF 304 SS PARTS WITH 316 SS.

THE UTILITY HAD NO CHANGE IN STATUS TO ANNOUNCE FOR THE

CURRENT REPORT PERIOD.
                                                                161
                                                                                        PEDCO ENVIRONMENTAL

-------
                  TABLE: 3
PERFORMANCE DESCRIPTION FOR OPERATIONAL F6D SYSTEMS  12/76
 IDENTIFICATION NO.
 UTILITY NAME
 UNIT NAME
 UNIT LOCATION
 UNIT RATING
 FUEL CHARACTERISTICS
 F6D VENDOR
 PROCtSS
 NEW OR RETROFIT
 START UP DATE
 F6D STATUS
 EFFICIENCY,
  PARTICULATES
 100

 RICKENBACKER AFB

 RICKENBACKER

 COLUMBUS  OHIO

   20 MW

 COAL 3.6 PERCENT. SULFUR

 RESEARCH COTTRELL

 LIME SCRUBBING

 RETROFIT

  3/76

 OPERATIONAL


 99 PERCENT
  S02
 90 PERCENT
 WATER MAKE UJ*
 SLUDGE DISPOSAL
 OPEN LOOP 2.50 GPrt/MW MAY
 UNSTABILIZED SLUDGE DISPOSED IN LINED POND
 UNIT COST
 OPERATIONAL
  EXPERIENCE
H10/KW CAPITAL
 REFER TO THE BACKGROUND INFORMATION SECTION IN TABLE 3 OF THIS REPORT.
 THE SCRUBBING SYSTEM WAS FIRST PLACED IN SERVICE MAKCH 11, 1976.
 THE SYSTEM SUPPLIER REPORTED THAT THE SYSTEM REMAINED OUT OF SERVICE
 THROUGHOUT THE MONTH OF NOVEMBER FOR COMPLETION OF REPAIRS TO
 THE SCRUBBER FAN THRUST BEARING.  THE SCRUBBEK WAS PUT BACK IN THE
 GAS STREAM AND REMAINED IN SERVICE THROUGHOUT THE MONTH.  A NEW
 STOKER BOILER* WHICH WILL REPLACE TWO OF THE OLDER UNITS, IS NOW
 BEING INSTALLED AT THIS FACILITY.
                                                            162
                                                                         PEOCO ENVIRONMENTAL

-------
                                                           BACKGROUND INFORMATION
                                                                     ON
                                                         RICKENBACKER AIR FORCE BASE
     IN 1971 RESEARCH-COTTRELL CONCLUDED AN AGREEMENT WITH A.B. BANCO VENTILATION, ENKOPING, SWEDEN.  THIS CONTRACTUAL ARRANGEMENT
ALLOWS RESEARCH-COTTRELL TO BE THE EXCLUSIVE LICENSEE OF THE BAHCO SULFUR DIOXIDE SCRUBBING PROCESS IN THE UNITED STATES.  TO
OATEi THERE ARE 19 SULFUR DIOXIDE BAHCO SCRUBBING SYSTEMS IN THE VARIOUS STAGES OF DEVELOPMENT THROUGHOUT THE WORLD.  THE FIRST
u.s. BAHCO INSTALLATION HANDLES SEVEN STOKER-TYPE COAL-FIRED BOILERS AT THE RICKENBACKCR AIR FORCE BASE IN COLUMBUS* OHIO.  THE
BOILERS ARE OLDER UNITS.  THREE WERE FIRST PLACED IN SERVICE IN 1952 AND THE REMAINING H CAME ON LINE IN 1954.  THE UMTS FIRE A
HIGH SULFUR COAL, 3.6 PERCENT SULFUR, AT HIGH COMBUSTION AIR RATESi 150 TO 160 PERCENT EXCESS AIR.
     THE RICKENBACKER EMISSION CONTROL SYSTEM CONSISTS ESSENTIALLY OF A MECHANICAL COLLECTOR, BAHCO SCRUBBER TOWER, LIME. STORAGE
AND HANDLING SYSTEM, CLARIFIERt BOOSTER FAN AND ASSOCIATED DUCTWORK. PUMPS, CONTROLS, AND A SLUDGE DISPOSAL POND.
     SOLID PARTICULATE AND SULFUR DIOXIDE-LADEN FLUE GAS TAKEN FROM EACH OF THE EXISTING SEVEN STACKS IS FED THROUGH A COMMON
HEADER AND INTO A MECHANICAL COLLECTOR WHERE PRIMARY PARTICULATE REMOVAL TAKES PLACE.  THE MECHANICAL COLLECTOR HAS A DESIGN
REMOVAL EFFICIENCY OF 70 PERCENT AND WAS INSTALLED PRIMARILY TO REDUCE FAN WEAR.  THE PARTLY CLEANED GAS THEN FLOWS TO THE FAN AND
INTO THE BAHCO TOWER WHERE ADDITIONAL PARTICULATE AND PRIMARY SULFUR DIOXIDE REMOVAL TAKES PLACE.
     THE BAHCO SCRUBBING VESSEL IS A VERTICAL TOWER CONSISTING OF TWO SCRUBBING STAGES.  GAS FLOWS THROUGH THE TOWER WHERE IS IS
CONTACTED WITH A LIME SLURRY SOLUTION.  AFTER PASSING THROUGH THE FIRST SCRUBBING STAGE, ENTRAINED MOISTURE IS REMOVED BY A
CYCLONIC TYPE MIST ELIMINATOR.  THE GAS THEN PASSES THROUGH A SECOND SCRUBBING STAGE AND A SECOND CYCLONIC TYPE MIST ELIMINATOR.
THE CLEANED GAS IS DISCHARGED TO THE ATMOSPHERE THROUGH A STACK MOUNTED DIRECTLY TO THE TOWER.
     PEBBLE LIME IS EMPLOYED AS THE REAGENT IN THE SCRUBBING SYSTEM AND IS PREPARED BY SLAKING AND DISSOLUTION IN A MIX/HOLD .TANK.
THE SCRUBBING SLURRY IS THEN PUMPED TO THE ABSORBER WHERE IT IS CONTACTED WITH THE FLUE GAS IN A COUNTERCURRENT FASHION.
     THE SPENT SCRUBBING SOLUTION IS DISCHARGED TO THE THICKENER WHERE THE WASTE SOLIDS SETTLE OUT. THICKENER OVERFLOW IS RETURNED
TO THE MIX/HOLD TANK.  THICKENER UNDERFLOW IS DISCHARGED TO A 5-ACRE HYPALON-LINED DISPOSAL POND.  THIS POND IS LOCATED APPROXI-
MATELY HOO FEET FROM THE SCRUBBING TOWER.  CLEAR WATER FROM THE POND IS RETURNED TO PROCESS AS SLAKING WATER.  A SIMPLIFIED
PROCESS FLO*. DIAGRAM OF THE RESEARCH COTTRELL/BAHCO WET LIME SCRUBBING SYSTEM IS PRESENTED IN FIGURE 19 OF APPENDIX C.
OPERATING HISTORY
                                                                                                  PEDCO ENVIRONMENTAL

-------
RICKENBACKER AFB (CONTINUED)
     THE: SYSTEM WAS INITIALLY PLACED IN SEKVICE MARCH n,  1976.  INITIAL OPERATION PROCEEDED IN AN OPEN WATER  LOOP nooE  BECAUSE
TH£ THICKENER WAS NOT YET COMPLETELY INSTALLED.  SULFUR DIOXIDE INLET CONCENTRATIONS WERE IN THE 1600  TO 2000  PPM RANGE.  HIGH
OXYGEN CONCENTRATIONS ALSO EXIST IN THE FLUE GAS BECAUSE THESE OLDERi INEFFICIENT BOILERS OPERATE AT 150 TO 160  PERCENT  EXCESS AIR
RATES.  SULFUR DIOXIDE REMOVAL EFFICIENCY HAS BEEN IN THE LOW 90 PERCENT PLUS RANGE.  LIME UTILIZATION HAS BEEN  VERY GOOD.
PROBLEMS ENCOUNTERED TO DATE HAVE BEEN PRIMARILY OF A MECHANICAL NATURE USUALLY ASSOCIATED WITH STARTUP.  THE  MAJOR PROBLEMS ARE
ITEMIZED BELOW.
          ELECTRICAL CIRCUITS ANt> SYSTEff CONTROL PANEL.
          PUMP MALFUNCTION - SPARE PARTS SHIPMENT DELAY.
          SEDIMENTATION BUILDUP IN THE SCRUBBER VESSEL (THIS WAS DUE PRIMARILY TO OPERATION AT HIGHER  THAN DESIGN SOLIDS CON-
          CENTRATION IN THE SCRUBBING SOLUTION BECAUSE THE THICKENER WAS NOT YET IN SERVICE PLUS GRIT  GETTING  THROUGH THE LIME
          SLAKER GRIT REMOVAL STEP).
          FAMILIARIZATION OF THE- OPERATING STAFF WITH THE MECHANICS OF THE PROCESS.
          I.D. BOOSTER FAN PROBLEMS.  ADDITIONAL BRACING. AND EPOXY GROUTING WAS REQUIRED TO STOP THE  ELEVATED FAN
          CONCRETE SUPPORT FRO* VIBRATING WHILE THE FAN WAS OPERATING.  A THRUST BEARING FAILURE IN THIS UWIT
          HAS ALSO BEEN ENCOUNTERED.
A NEW COAL-FIRED STOKER-TYPE BOILER (RILEY STOKER. 60 MM BTU/HR. HEAT CAPACITY). IS NOW BEING INSTALLED AT THIS FACILITY.  THE
INSTALLATION OF THIS NEW UltIT WILL RESULT IN THE TERMINATION OF OPERATIONS FOR THE NO. 1 AND 2 UNITS AND STANDBY SERVICE FOR THE
NO. 3 UNIT.  THESE ARE THE THREE OLDER UMTS (MANUFACTURED AND INSTALLED IN 1952) WHICH ARE OPERATING AT HIGH EXCESS AIR RATES AND
CORRESPONDING LOW THERMAL EFFICIENCIES.  THE OVERALL RESULT SHOULD BE A STABILIZATION OF FLUE GAS CONDITIONS,  INCREASED SCRUBBER
EFFICIENCY. AND REDUCTION OF CAftBOW FlNCS CARRYOVER STEMWIN& FRGff THE INEFFICIENT COMBUSTION CONDITIONS IN THESE OLDER UWITS.
     THE BAHCO FGD CONTROL SYSTEIt Ola NO? OPERATE DURING NOVEMBER BECAUSE OF COMPLETION OF REPAIRS TO THE 1.0. FAN HOUSING.
THE STSTEK OPERATED DURING THE- ENTIRE MOWtH OF DECEMBER WITH S02 REMOVAL EFFICIENCY VARYING FROM 85 TO 90 PERCENT.  LIME FEED
HAQ TO PROCEED ON ft MANUAL BASIS BECAUSE OF A MALFUNCTIONING SLftKER.  THE NEW STOKER BOILER HAS NOT YET BEEN PLACED IN COMMERCIAL
OPERATION, PRIMARILY BECAUSE 6F PRGStEMS RELATED TO SEVERE WEATHER CONTITIONS.
                                                                                                  PEDCO ENVIRONMENTAL

-------
                  TABLE 5
PERFORMANCE DESCRIPTION FOR OPERATIONAL FGD SYSTEMS  12/76
 IDENTIFICATION NO.
 UTILITY NAME
 UNIT NAME
 UNIT LOCATION
 UNIT RATING
 FUEL CHARACTERISTICS
 FGD VENDOR
 PROCESS
 NEW OR RETROFIT
 START UP DATE
 FGO STATUS
 EFFICIENCY.
  PARTICULATES

  S02
 WATER HAKE UP
 SLUDGE DISPOSAL
 UNIT COST
 OPERATIONAL
  EXPERIENCE
112
TENNESSEE VALLEY AUTHORITY
SHAWNEE NO.IDA
PADUCAH KENTUCKY
  10 HW
COAL 2.9 PERCENT SULFUR
UNIVERSAL OIL PRODUCTS
LIME/LIMESTONE SCRUBBING
RETROFIT
 H/72
OPERATIONAL
REFER TO BACKGROUND INFORMATION SECTION IN TABLE 3 OF THIS REPORT. THIS
TURBULENT CONTACT ABSORBER(TCA) LIME/LIMESTONE SCRUBBING SYSTEM HAS BEEN
OPERATIONAL SINCE APRIL 1972. THIS TEST PROGRAM IS FUNDED BY THE EPA.
TVA IS THE CONSTRUCTOR AND FACILITY OPERATOR. THE BECHTEL CORP. OF SAN
FRANCISCO IS THE MAJOR CONTRACTOR* TEST DIRECTOR, AND REPORT WRITER.
                                                            185
                                                                        PEDCO ENVIRONMENTAL

-------
                  TABLE 3
PERFORMANCE DESCRIPTION FOR OPERATIONAL F60 SYSTEMS  12/76
 IDENTIFICATION NO.
 UTILITY NAME
 UNIT NAME
 UNIT LOCATION
 UNIT RATING
 FUEL CHARACTERISTICS
 F6D VENDOR
 PROCESS
 NEW OR RETROFIT
 START UP DATE
 FGD STATUS
 EFFICIENCY,
  PARTICULATES

  S02

 WATER MAKE UP

 SLUDGE DISPOSAL
 UNIT COST
113
TENNESSEE VALLEY AUTHORITY
SHAWNEE N0.10B
PAOUCAH KENTUCKY
  10 MW
COAL 2.9 PERCENT .SULFUR
GHEMICO
LIME/LIMESTONE SCRUBBING
RETROFIT
 4/72
OPERATIONAL
 OPERATIONAL
  EXPERIENCE
REFER TO BACKGROUND INFORMATION SECTION IN TABLE 3 OF THIS REPORT. THIS
VENTURI/SPKAY TOWER LIME/LIMESTONE SCRUBBING SYSTEM HAS BEEN OPERATIONAL
SINCE APRIL 1972. THIS TEST PROGRAM IS FUNDED BY THE EPA. TVA IS THE
CONSTRUCTOR AND FACILITY OPERATOR. THE BECHTEL CORP. OF SAN FRANCISCO IS
THE MAJOR CONTRACTOR,TEST DIRECTOR, AND REPORT WRITER.
                                                                                               PEOCO ENVIRONMENTAL

-------
                                                            BACKGROUND
                                                                      ON
                                                       SHAWNEE NOS. 10A, lOBt AND IOC
     IN JUNE I966t THE EPA INITIATED A PROGRAM TO TEST PROTOTYPE LIME AND LIMESTONE SYSTEMS FOR REMOVAL OF SULFUR DIOXIDE AND
PARTICIPATES FROM COAL-FIRED BOILER FLUE GASES.  THE PROGRAM WAS CARRIED OUT IN A TEST FACILITY INCORPORATED INTO THE FLUE GAS
DUCTWORK OF UNIT NQ. 10, A COAL-FIRED BOILER AT THE TVA SHAWNEE POWER STATION* PADUCAH, KENTUCKY.   TVA IS THE CONSTRUCTOR AND
FACILITY OPERATOR* BtCHTEL CORP. IS THE MAJOR CONTRACTOR, TEST DIRECTOR, AND REPORT WRITER.
     THE TEST FACILITY CONSISTS OF THREE PARALLEL SCRUBBER SYSTEMS OF PROTOTYPE SIZE, TREATING PART OF THE FLUE GAS FROM THE
BOILER.  EACH SCRUBBER TRAIN IS CAPABLE OF TREATING APPROXIMATELY 30,000 ACFM OR THE EQUIVALENT OF APPROXIMATELY 10 MW OF POWER
PLANT GENERATING CAPACITY.
     THREE PARALLEL WET SCRUBBER SYSTEMS WERE SELECTED FOR THE TEST PROJECT*  D A VENTURI WITH A SPRAY TOWER AFTER ABSORBER* 2>  A
TURBULENT CONTACT ABSORBER (TCA) AND 3) A MARBLE-BED ABSORBER.  THE VENTURI SYSTEM, MANUFACTURED BY CHEMICAL CONSTRUCTION CO.,
CONTAINS AN ADJUSTABLE THROAT THAT PERMITS CONTROL AND VARIATION OF PRESSURE DROP UNDER A WIDE RANGE OF FLOW CONDITIONS.  THE TCA
UNIT, MANUFACTURED BY UNIVERSAL OIL PRODUCTS, INCORPORATES A FLUIDIZED BED OF LOW DENSITY PLASTIC SPHERES THAT ARE FREE TO MOVE
BETWEEN RETURNING GRIDS.  THE MARBLE-BED ABSORBER, SUPPLIED BY COMBUSTION ENGINEERING CO,t USES A PACKING OF 3/4-INCH GLASS MARBLE
SPHERES AND A TURBULENT LAYER OF LIQUID AND GAS ABOVE THE MARBLE LAYER TO ENHANCE MASS TRANSFER.
     IN JUNE 1974, THE EPA BEGAN A 3-YEAR ADVANCED TEST PROGRAM AT THE SHAWNEE FACILITY WITH THESE MAJOR GOALS*  (1) CONTINUA-
TION OF LONG-TERM TESTING, WITH EMPHASIS PLACED UPON THE RELIABLE OPERATION OF MIST ELIMINATION SYSTEMS AT INCREASED GAS VELOCITY,
(2) INVESTIGATION OF ADVANCED PROCESS AND EQUIPMENT DESIGN VARIATIONS FOR IMPROVING SYSTEM RELIABILITY AND PROCESS ECONOMICS, AND
(3) LONG-TERM RELIABILITY TESTING ON PROMISING PROCESS AND EQUIPMENT DESIGN VARIATIONS.
     THE TWO PARALLEL SCRUBBING SYSTEMS OPERATING DURING THE ADVANCED PROGRAM ARE THE VENTURI/SPRAY TOWER SYSTEM AND THE TCA UNIT.
GENERAL PROCESS FLOW DIAGRAMS OF THE TWO PROTOTYPE UNITS ARE PROVIDED IN FIGURES 20 AND 21 OF APPENDIX C.  OPERATION OF THE
MARBLE-BED ABSORBER UNIT HAS BECN PERMANENTLY DISCONTINUED.
     EACH OF THE SCRUBBING SYSTEMS CONTAINS ITS OWN SLURRY HANDLING FACILITIES AND CAN TREAT APPROXIMATELY 30,000 ACFM OF GAS AT
300 F CONTAINING 1600 TO 4000 PPN OF SULFUR DIOXIDE AND 2 TO * GRAINS/SCF OF PARTICULARS.  BOILER NO. 1 NORMALLY BURNS A HIGH-
SULFUR BITUMINOUS COAL.
                                                               167                                PEDCO ENVIRONMENTAL

-------
SHAWNEE NOS. IDA, 108t AND IOC (CONTINUED)



     FROM JUNE 197H TO JANUAKY, 1976. MIST  ELIMINATION AND LIMESTONE UTILIZATION TESTS WERE CONDUCTED AT THE SHAWNEE FACILITY.



DURING THIS TEST PERIOD THE VENTURI/SPRAT TOWER SYSTEM WAS OPERATED ON BOTH LIME AND LIMESTONE AND THE TCA SYSTEM WITH LIMESTONE,



TESTING WAS PERFORMED UNDER A CLOSED-WATER-LOOP OPERATION MODE.  DURING THIS PERIOD THE SLURRY SOLIDS CONTAINED APPROXIMATELY 40



TO 50 PERCENT WEIGHT FLY ASH BECAUSE OF RELATIVELY HIGH GAS INLET PARTICULATE LOADING.  THIS TESTING PROGRAM IS SCHEDULED TO RUN



THROUGH TO JUNE 1977.



     ADDITIONAL INFORMATION AND DATA CONCERNING THE DETAILS OF THE ADVANCED TEST PROGRAM ARE PRESENTED IN THE PERFORMANCE TABLE



THAT FOLLOWS.
                                                               168                                PEDCO  ENVIRONMENTAL

-------
                                                          SHAWNEE MOS. 10A AND 10B
                    FGO SYSTEM OPERATING HOURS
TEST RUN PERIOD        IDA          10B                                              COMMENTS
SEP. 75                                      THIS EXPERIMENTAL ERA-FUNDED OPERATION IS PROCEEDING WITH THE TEST PROGRAM.  TWO
OCT. 75                                      ABSORBER MODULES ARE CURRENTLY OPERATIONAL (10 MW EACH)* THE MARBLE-BED ABSORBER
                                             IS STILL INOPERATIVE (SINCE -JULY 1973)*  CURRENT EXPERIMENTS ARE RELATED TO MIST
                                             ELIMINATOR SECTION.
NOV. 75                                      RECENT TESTING AT SHAWNEE HAS SHOWN THAT THE CHEVRON MIST ELIMINATORS IN BOTH THE
DEC. 75                                      SPRAY TOWER AND THE TCA CAN BE KEPT FREE OF SOLIDS BUILDUP AT HIGH ALKALI UTILIZATION
                                             GREATER THAN 90 PERCENT, USING ONLY INTERMITTENT WASHING WITH AVAILABLE RAW WATER.
                                             THIS HIGH UTILIZATION IS NORMALLY ACHIEVED WITH LIME* IT HAS BEEN ACHIEVED WITH
                                             LIMESTONE AT REDUCED SCRUBBER INLET SLURRY PH (ABOUT 5.2) AND WITH THREE EFFLUENT
                                             TANKS IN SERIES TO SIMULATE A PLUG-FLOW REACTOR.
                                             TESTING IS CONTINUING TO DETERMINE THE EFFECTS OF PROCESS VARIABLES ON MIST ELIMINA-
                                             TOR PERFORMANCE AND ON LIMESTONE UTILIZATION.  FUTURE PLANS INCLUDE*  (1) FACTORIAL
                                             TESTING WITH LIME AND LIMESTONE TO DETERMINE THE EFFECTS OF PROCESS VARIABLES ON S02
                                             REMOVAL AND (2) TESTING THE OXIDATION OF SLUDGE TO GYPSUM IN THE VENTURI/SPRAY TOWER
                                             SYSTEM USING AIR SPARGING OF AN ACIDIFIED SLURRY BLEED STREAM.
JAN. 76                                      THE ADVANCED TEST PROGRAM IS CONTINUING.  HIGHLIGHTS OF THE PROGRAM ARE AS FOLLOWS*
                                                  EVALUATE SCRUBBER OPERABILITY DURING VARIABLE LOAD OPERATION.
                                                  CONTINUE LONG-TERM RELIABILITY TESTING.
                                                  INVESTIGATE METHODS FOR IMPROVING WASTE SOLIDS SEPARATION.
                                                  CONTINUE SLUDGE OXIDATION AND SLUDGE FIXATION STUDY PROGRAMS.
                                                  EVALUATE SYSTEM PERFORMANCE AT REDUCED FLY ASH LOADINGS.
                                                  DETERMINE THE PRACTICAL UPPER LIMITS OF S02 REMOVAL EFFICIENCY.
                                                  EVALUATE AOOITITION OF MAGNESIUM ION TO THE SCRUBBING SLURRY.
                                                       CHARACTERIZE ALL STACK GAS EMISSION COMPONENTS.
                                                       EVALUATE MATERIALS OF CONSTRUCTION OF ALL SCRUBBER AND PLANT-RELATED
                                                       COMPONENTS.
                                                               169                                PEDCO ENVIRONMENTAL

-------
                                               SHAWNEE NOS.  IDA AND 10B (CONTINUED)
                    FGD SYSTEM OPERATING HOURS
TEST RUN PERIOD        IOA          IOB                                              COMMENTS
                                                       DEVELOP A COMPUTER PROGRAM FOR DESIGN AND  COST  ANALYSIS  OF  FULL-SCALE
                                                       LIME/LIMESTONE  SYSTEM.
MAR. 76                                           BECHTEL REPORTED THAT THE FACTORIAL TEST PROGRAM,  EVALUATING  THE PERFORMANCE
APR. 76                                           OF THE LIME/LIMESTONE SCRUBBING SYSTEMS WITH AND WITHOUT  MAGNESIUM ADDITION
                                                  HAS BEEN COMPLETED.   CURRENTLY, TESTING IS PROCEEDING  ON  THE  EVALUATION  OF
                                                  SYSTEM PERFORMANCE AS A FUNCTION OF LOU RESIDENCE  TIMES  (1.5  TO  5.0 MINUTES)
                                                  IN THE RECYCLE TANKS.  IN ADDITION, A FLY ASH-FREE DUCT  IS  BEING INSTALLED
                                                  AT THE TEST FACILITY, THUS ENABLING EVALUATION  OF  SYSTEM  PERFORMANCE IN  THE
                                                  ABSENCE OF FLY ASH.
MAY  76                                           THE TEST DIRECTOR, BECHTEL,  PROVIDED THE FOLLOWING INPUT  CONCERNING THE
JUN. 76                                           OPERATION OF THE EXPERIMENTAL SCRUBBING SYSTEMS DURING THE  REPORT PERIOD*
                                                       THE EFFECT OF MGO ADDITION WAS EXPLORED IN BOTH SCRUBBER SYSTEMS.   RESULTS
                                                       INDICATE MAGNESIUM ION IN THE SCRUBBER  SLURRY LIQUOR ENCHANCES S02  REMOVAL
                                                       AND CAN DEPRESS SULFATE SUPERSATURATION.  IT  WAS  FOUND THAT THE MAGNESIUM
                                                       ION CONCENTRATION HAD TO EXCEED THE EQUIVALENT  CHLORIDE  ION CONCENTRATION
                                                       TO HAVE AN EFFECT ON S02 REMOVAL.
                                                       IN THE TCA UNIT, WITH LIMESTONE SLURRY*  S02 REMOVAL  WAS  INCREASED FROM 75
                                                       TO 95 PERCENT BY INCREASING THE MAGNESIUM  ION CONCENTRATION TO 9,000 PPM IN
                                                       EXCESS OF EQUIVALENT CHLORIDE ION.  TO  ACHIEVE  THIS  CONCENTRATION LEVEL,
                                                       MAGNESIUM OXIDE WAS ADDED AT A RATE EQUAL  TO  6  PERCENT BY WEIGHT OF THE
                                                       LIMESTONE ADDITION RATE.
                                                       IN THE VENTURI/SPRAY TOWER SYSTEMS, WITH LIME SLURRY,  S02 REMOVAL WAS
                                                       INCREASED FROM  75 TO 90 PERCENT BY INCREASING MAGNESIUM  ION CONCENTRATION
                                                       TO 2.000 PPM IN EXCESS OF EQUIVALENT CHLORIDE ION.   THE  MAGNESIUM OXIDE
                                                       ADDITION RATE WAS 2 PERCENT BY WEIGHT OF THE  LIME ADDITION  RATE.

                                                               190                               PEOCO  ENVIRONMENTAL

-------
                                               SHAWNEE NOS. IDA AND 108 (CONTINUED)

                    F6D SYSTEM OPERATING HOURS
TEST RUN PERIOD        IDA          10B                                              COMMENTS

                                                       BOTH SCRUBBING SYSTEMS OPERATED IN THE SUBSATURATED SULFATE MODE WHEN

                                                       MAGNESIUM OXIDE WAS ADDED.  INLET S02 CONCENTRATIONS DURING THE TESTS

                                                       AVERAGE APPROXIMATELY 3,000 PPM DURING THESE TESTS.

                                                       FOLLOWING THE TEST BLOCKS MENTIONED ABOVE, BOTH SCRUBBERS ARE OPERATING

                                                       WITH LIME SLURRY SCRUBBING SOLUTIONS, THE TCA SYSTEM ON FLUE GAS CONTAINING

                                                       FLY ASH AND THE VENTURI/SPRAY TOWER SYSTEM ON FLY ASH-FREE FLUE GAS.

JUL. 76                                           EXPERIMENTAL OPERATION OF THE EPA/TVA ALKALI SCRUBBING TEST FACILITY CONTINUED

AUG. 76                                           DURING THE REPORT PERIOD.  BECHTELt THE TEST DIRECTOR, PROVIDED THE FOLLOWING

                                                  INPUT CONCERNING THE OPERATION OF THE PROTOTYPE TEST UNITS.

                                                       VENTURI/SPRAY TOWER SYSTEM*  THIS SYSTEM OPERATED ON FLY ASH-FREE FLUE GAS

                                                       USING A LIME SLURRY SCRUBBING SOLUTION.  NO SIGNIFICANT DIFFERENCES IN S02

                                                       REMOVAL, GYPSUM SATURATION AND SU|_FITE OXIDATION WERE DETECTED (VERSUS FLY

                                                       ASH-LADEN  FLUE GAS).  ONE DIFFERENCE NOTED WAS THE FILTER CAKE SOLIDS

                                                       CONTENT WHICH WAS APPROXIMATELY 10 PERCENT LOWER FOR THE FLY ASH-FREE

                                                       SLUDGE (40 TO 50 PERCENT SOLIDS) VERSUS THE FLY ASH-LADEN SLUDGE (50 TO 60

                                                       PERCENT SOLIDS).  IN ADDITION, OPERATION IN A LOW RESIDENCE TIME MODE (3-

                                                       MINUTES) WAS EXPLORED.  SCALE FREE OPERATION WAS ACHIEVED IN THIS MODE

                                                       UNDER THE FOLLOWING CONDITIONS*  8 PERCENT SOLIDS  (NO FLY ASH) IN THE

                                                       RECIRCULATEO SLURRY* PH OF THE SCRUBBER LIQUOR INLET WAS 8.0* SUPERFICIAL

                                                       GAS VELOCITY OF 9.4 FT./SFC.* AND A TOTAL LIQUID GAS RATION (L/G) OF 71

                                                       GAL./MCF).  SOME SCALE FORMATION OCCURRED WHEN THE SOLIDS CONTENT IN THE

                                                       RECIRCULATED SLURRY DROPPED BELOW THE 
-------
                                               SHAWNEE NOS.  10A  AND  10B  (CONTINUED)
                    FGO SYSTEM OPERATING HOURS
TEST RUN PERIOD        10A          10B                                              COMMENTS
                                                       PPM*  SUPERFICIAL  GAS  VELOCITY  WAS  12.5 FT./SEC.* L/G WAS 50* THE SCRUBBING
                                                       SOLUTION  INLET  PH WAS 7.0*  AND RESIDENCE  TIME MAS  t»MINUTES.  THE  S02
                                                       REMOVAL EFFICIENCY WAS APPROXIMATELY  90 PERCENT.   WHEN  THE  L/G  WAS REDUCED
                                                       TO 37,  WHILE  ALL  OTHER CONDITIONS  REMAINED  CONSTANT, SEVERE GYPSUM SCALE
                                                       FORMATION RESULTED.  INCREASING THE EFFECTIVE MAGNESIUM ION CONCENTRATION
                                                       TO 4000 PPM AND THE SCRUBBER LIQUOR INLET PH TO 8.0 DID NOT AMELIORATE  THE
                                                       SCALE PROBLLEH.  PRESENTLY, THE VENTURI/SPRAY TOWER SYSTEM  IS OPERATING ON
                                                       FLY ASH-FREE  FLUE GAS WITH  A MAGNESIUM OXIDE INNOCULATEO LIME SCRUBBING
                                                       SLURRY.
SEP. 76                                           IN SEPTEMBER AND OCTOBER 1976, THE  VENTURI/SPRAY SYSTEM WAS  OPERATED WITH FLY
OCT. 76                                           ASH-FREE FLUE  GAS  USING LIME SLURRY WITH ADDED MAGNESIUM OXIDE.  TYPICAL TEST
                                                  CONDITIONS WERE 9.H  FT/SEC SPRAY TOWER  GAS VELOCITY, 21 GAL/MCF  VENTURI L/S, 50
                                                  GAL/MCF SPRAY  TOWER  L/G* 8 PERCENT  SLURRY  SOLIDS (FLY ASH-FREE), 3 MINUTES
                                                  RESIDENCE  TIME, 7.0  SCRUBBER INLET  PH,  AND 2000  PPM EFFECTIVE MG ION CONCENTRA-
                                                  TION (I.E.,  EXCESS OVER EQUIVALENT  CHLORIDE ION).  RESULTS WERE  NOT  CONSISTENT
                                                  AT THE CONDITIONS.  DURING ONE PERIOD,  SCRUBBING INLET  LIQUOR GYPSUM SATURA-
                                                  TION AVERAGED  85 PERCENT WITH 80 PERCENT S02 REMOVAL AND WITH SOME GYPSUM
                                                  SCALE FORMATION. IN  A  LATER PERIOD, AT  SEEMINGLY IDENTICAL TEST  CONDITIONS,
                                                  GYPSUM SATURATIONS DROPPED TO 10 PERCENT WITH  98 PERCENT 802 REMOVAL AND THE
                                                  SCRUBBER DESCALED. A SEVEN-WEEK  PROGRAM OF INTENSIVE FLUE GAS CHARACTERIZATION
                                                  TESTING WAS  STARTED  IN MID-OCTOBER  ON THE  VENTURI/SPRAY TOWER SYSTEM. THESE
                                                  TESTS ARE  BEING HADE TO MEASURE  SIMULTANEOUS INLET AND  OUTLET FLUE GAS  PART.
                                                  MASS LOADING,  PARTICULATE  SIZE DISTRIBUTION. AND GASEOUS S03 CONCENTRATION.
                                                  THE TCA SYSTEM CONTINUED TO OPERATE DURING THIS  PERIOD  ON FLY ASH-LADEN FLUE GAS
                                                  USING LIME SLURRY  WITH ADDED MAGNESIUM  OXIDE.  THE TEST RESULTS  SO FAR  INDICATED
                                                  THAT THE DEGREE OF SuLFATE (GYPSUM) SUB-SATURATION
                                                              192                                PEOCO ENVIRONMENTAL

-------
                                               SHAWNEE NOS. IDA AMD 10B (CONTINUED)



                                                  IS A SENSITIVE FUNCTION OF THE EFFLUENT RESIDENCE TIME AND THE APPEARS TO BE AN



                                                  OPTIMIM RESIDENCE TIME AT WHICH MINIMUM SULFATE (GYPSUM) SUBSATURATION OCCURS.



                                                  TYPICAL CONDITIONS* GAS VELOCITY 12.5 FT/SEC , L/6 OF 50,PH OF 7.0, 2000 PPM OF



                                                  MG ION, AND 6 PERCENT SOLIDS. AT THESE CONDITIONS GYPSUM SATURATIONS WERE 95, 50



                                                  AND 92 PERCENT, AT RESIDENCE TIMES OF 3tf< AND MINUTES, RESPECTIVELY. FURTHER



                                                  TEST WERE RUN AT 37 GAL/MCF L/G AND 6/0 SCRUBBER INLET PH WITH OTHER CONDITIONS



                                                  THE SAME.  DURING THESE TESTS GYPSUM SATURATIONS WERE 95, 95* so* AND 90 PERCENT



                                                  AT 3,»



                                                  GAS FLOW RATE  (20,00 TO 35,000 ACFM). SPRAY TOWER LIQUOR RATE (0 TO 1400



                                                  GPM) AND VENTURI PRESSURE DROP (3 TO 9 IN. H20). WITH H TO 6 GR/DSCF



                                                  PART1CULATE AT THE INLET, TYPICAL OUTLET LOADINGS WERE 0.02 TO 0.04



                                                  GR/DSCF. WHEN THE ESP WAS IN SERVICE, THE SCRUBBER OUTLET LOADING AVERAGED



                                                  LESS THAN 0.005 GR/DSCF. SIZE DISTRIBUTION ANALYSIS IS PROCEEDING.



                                                  ACID MIST VALUES WERE APPROXIMATELY 2 TO 25 PPM AT THE SCRUBBER  INLET



                                                  WITH REMOVAL IN THE 50 TO 75 PERCENT RANGE. DURING THE REMAINDER OF



                                                  THE MONTH THE UNIT WAS DOWN FOR MODIFICATIONS FOR 2-STAGE OXIDATION



                                                  TESTING  (SEC FIGURE 2  -A IN APPENDIX C>. FLY ASH-FREE AND LADEN FLUE



                                                  GAS TESTING WITH LIME AND AND LIMESTONE SLURRIES WERE CONDUCTED DURING



                                                  THE PERIOD ON THE TCA UNIT. MAGNESIUM OXIDE WAS NOT ADDED TO THE SLURRIES.
                                                               193                                PEOCO ENVIRONMENTAL

-------
19H                                PCOCO ENVIRONMENTAL

-------
            TABLE  *




NUMBER AND TOTAL HW OF FGO SYSTEMS
                 195                PEDCO-ENVIRONMENTAL

-------
196                                PEOCO ENVIRONMENTAL

-------
               TABLE H
NUMBER AND TOTAL MW OF FG0 SYSTEMS
      STATUS



   OPERATIONAL

   UNDER CONSTRUCTION

   PLANNING
     CONTRACT AWARDED
                           NO.OF
                           UNITS
                             30

                             31
                             20

LETTER OF INTENT              2

REQUESTING/EVALUATING BIDS    H

CONSIDERING ONLY FGD SYSTEMS 37

TOTAL                       12*
 MM




 6H59.

13309.


 9981.

  3t»5.

 2327.

16726.

H9167.
                                                       197
                                                                                    PEDCO  ENVIRONMENTAL

-------
19d                                PEDCO  ENVIRONMENTAL

-------
            TABLE  5




SUMMAKY OF FGD SYSTEMS BY COMPANY
                  199                PEDCO-ENVIRONMENTAL

-------
200                                PEOCO ENVIRONMENTAU

-------
                                         TABLE 5
                                SUMMARY OF FGD SYSTEMS  BY  COMPANY
         UTILITY

ALABAMA ELECTRIC COOP
ALLEGHENY POWER SYSTEM
ARIZONA ELECTRIC POWER COOP
ARIZONA PUBLIC SEhVlCE
BASIN ELECTRIC PO»ER COOP
BIG RIVtKS ELECTRIC COOP CORP.
BRAZOS ELECTRIC POWER COOP
CENTRAL ILLlfcOIS LIGHT CO.
CEN1KAL ILLINOIS PUBLIC SERV
CINCINNATI GAS & ELECTRIC CO.
COLORADO UTE ELECTRICAL ASSN.
COLUMBUS & SOUTHERN OHIO ELEC.
COMMONWEALTH EDISON
DETROIT EDISON
DUOUESNE LIGHT
EASTERN KENTUCKY POWER COOP
GENERAL MOTORS
GULF POWER CO.
INDIANAPOLIS POWER & LIGHT CO.
KANSAS CITY POWER & LIGHT
KANSAS POWER £ LIGHT
KENTUCKY UTILITIES
KEY WEST UTILITY BOARD
LOUISVILLE GAS & ELECTRIC
MINNESOTA POWER AND LIGHT co.
KINNKOTA POWER COOPERATIVE
MONTANA POWER CO.
NEVADA POWER
NEW ENGLAND ELEC SYSTEM
NIAGARA MOHAWK POWER COOP.
NORTHERN INDIANA PUB SERVICE
NORTHERN INDIANA PUBLIC SERVIC
NORTHERN STATES POWER CO.
OTTER TAIL POWER COMPANY
PACIFIC POWER AND LIGHT CO.
PENNSYLVANIA POWER CO.
PHILADELPHIA ELECTRIC co.
POTOMAC ELECTRIC & POWER
PUBLIC SERVICE CO OF COLORADO
PUBLIC SERVICE CO OF NEW MEX.
PUBLIC SERVICE OF INDIANA
RICKENBACKER AFB
SALT KIVER PROJECT
SOUTH CAROLINA PUBLIC SERVICE
TAT AI nprPATTnfDAt
1 v 1 Al- Ur C**H 1 lUl>iA&»

WWIVM 1 F»wi* 1 A WI*
CONTRACT
AWARDED
NO.
2
2
2
5
5
1
1
3
1
1
2
4
2
1
2
1
1
1
2
3
4
1
1
8
1
1
4
10
1
1
2
1
4
1
1
3
if
2
1

-------
                                         TABLE 5
                                SUMMARY OF FGD SYSTEMS BY COMPANY
         UTILITY

SOUTHERN CALIFORNIA EDISON
SOUTHERN ILLINOIS POWER COOP
SOUTHERN INDIANA GAS&ELECTRIC
SOUTHERN MISSISSIPPI ELECTRIC
SPRINGFIELD CITY UTILITIES
TENNESSEE VALLEY AUTHORITY
TEXAS UTILITIES CO.
UNITED POWER ASSOCIATION
UTAH POWER & LIGHT CO.
WISCONSIN POWER & LIGHT CO.
TfiT Al ftPF*R AT TfllUAl
1 v I AL U"C.f»M 1 AUnlAi-

fewm^ • nww , * w*«
CONTRACT
AWARDED
NO.
2
1
1
2
1
3
5
2
2
1
MW
1410.
184.
2bO.
360.
200.
570.
3922.
1090.
615.
527.
NO.
0
0
0
0
0
2
0
0
0
0
MW
0.
0.
0.
0.
0.
20.
0.
0.
0.
0.
NO.
0
0
0
2
1
1
3
0
1
0
MW
0.
0.
0.
360.
200.
550.
2336.
0.
415.
0.
NO.
0
1
1
0
0
0
2
2
1
0
MW
0.
184.
250.
0.
0.
0.
1586.
1090.
400.
0.

LETTER OF REQUESTING/
INTENT
NO.
0
0
0
0
0
0
0
0
0
0
MW
0.
0.
0.
0.
0.
0.
0.
0.
0.
0.
EVAL.
NO.
0
0
0
0
0
0
0
0
0
1
BIDS
MW
0.
0.
0.
0.
0.
0.
0.
0.
0.
527.
CONSIDERING
FGD
NO.
2
0
0
0
0
0
0
0
0
0
SYSTEMS
HW
1410.
0.
0.
0.
0.
0.
0.
0.
0.
0.
   TOTALS
124  49167.   30   6459.   31  13309.   20   9981,
365.
2327.   37  16726,
                                                              202
                                                              PEDCO ENVIRONMENTAL

-------
           TABLE  b




SUMMARY OF FGD SYSTEMS BY VENDOR
                203                 PEDCO-ENVIRONMENTAL

-------
204                                PEDCO ENVIRONMENTAL

-------
           TABLE 6
SUMMARY OF FGD SYSTEMS BY VENDOR

TOTAL
MANUFACTURER/PROCESS
AOL/COMBUSTION EQUIP ASSOCIATE
LIKE/ALKALINE FLYASH SCRUBBING
SODIUM CARBONATE SCRUBBING
TOTAL* ADL/COMBUSTiON EQUIP ASS
AMERICAN AIR FILTER
LIME SCRUBBING
TOTAL, AMERICAN AIR FILTER
BABCOCK & WILCOX
LIMESTONE SCRUBBING
TOTAL, BABCOCK & WILCOX
BABCOCK AND WILCOX
LIME SCRUBBING
TOTAL, BABCOCK AND WILCOX
BUELL/ENVIROTECH
DOUBLE ALKALI SCRUBBING
TOTAL, BUELL/ENVIROTECH
CHEMICO
LIME SCRUBBING
LIME/LIMESTONE SCRUBBING
LIMESTONE SCRUBBING
TOTAL, CHEMICO
CHIYOOA INTERNATIONAL
THOROUGHBRED 101
TOTAL, CHIYODA INTERNATIONAL
COMBUSTION ENGINEERING
LIME SCRUBBING
LIMESTONE INJECTION AWET SCRUB
LIMESTONE SCRUBBING
TOTAL, COMBUSTION ENGINEERING
DAVY POWERGAS/ALHEO CHEMICAL
WELLMAN LORD/ALLIED CHEMICAL
TOTAL, DAVY POWERGAS/ALLIED CHE
NO.

3
3
6

4
H

3
3

2
2

1
1

5
1
1
7

1
1

2
4
4
10

3
3
MW

1170.
375.
15H5,

917.
917.

1267.
1267.

1250.
1250.

575.
575.

3005.
10.
750.
3765.

23.
23.

248.
765.
2750.
3763.

830.
830.
OPERATIONAL CONSTRUCTION
NO.

2
3
5

2
2

2
2

0
0

0
0

3
1
0
4

1
1

1
4
1
6

0
0
MW

720.
375.
1095.

242.
242.

987.
987.

0.
0.

0.
0.

1755.
10.
0.
1765.

23.
23.

65.
765.
710.
1540.

0.
0.
NO.

1
0
1

2
2

1
1

2
2

1
1

2
0
1
3

0
0

. 1
0
3
4

3
3
MU

450.
0.
450.

675.
675.

280.
280.

1250.
1250.

575.
575.

1250.
0.
750.
2000.

0.
0.

183.
0.
2040.
2223.

830.
830.
                                    205
PEOCO ENVIRONMENTAL

-------
           TABLE 6
SUMMARY OF FGO SYSTEMS BY VENDOR
TOTAL
MANUFACTURER/PROCESS
KOCH/GENERAL MOTORS
DOUBLE ALKALI SCRUBBING
TOTAL « KOCH/GENERAL MOTORS
PEABOOY ENGINEERING
LIMESTONE SCRUBBING
TOTAL, PEABODY ENGINEERING
RESEARCH COTTRELL
LIME SCRUBBING
LIMESTONE SCRUBBING
TOTAL, RESEARCH COfTRELL
RILEY STOKER / ENVIRONEERING
LIMESTONE SCRUBBING
TOTAL, RILEY STOKER / ENVIRONEE
SO. CALIFORNIA EDISON
LIME SCRUBBING
TOTAL, SO. CALIFORNIA EDISON
TENNESSEE VALLEY AUTHORITY
LIMESTONE SCRUBBING
TOTAL, TENNESSEE VALLEY AUTHOR I
UNITED EftGXNEERS / PECO
MAGNESIUM OXIDE SCRUBBING
TOTAL, UNITED ENGINEERS / PECO
UNIVERSAL OIL PRODUCTS
LIME SCRUBBING
LIME/LIMESTONE SCRUBBING
LIMESTONE SCRUBBING
TOTAL, UNIVERSAL OIL PRODUCTS
UOP / PUB SERVICE OF COLORADO
LIMESTONE SCRUBBING
TOTAL, UOP / PUB SERVICE OF COL
ZURN AIR SYSTEMS
LIMESTONE SCRUBBING
TOTAL, ZURN AIR SYSTEMS
NO.

1
1

3
3

1
6
7

if
4

1
1

1
1

1
1

1
1
2
4

1
1

1
1
MW

32.
32.

613.
613.

20.
2361.
2371.

760.
760.

160.
160.

550.
550.

120.
120.

400.
10.
730.
1140.

50.
50.

37.
37.

OPERAT]
NO.

1
1

1
1

1
1
2

1
1

1
1
*
0
0

1
1

0
1
0
1

1
1

1
1
— STATU
:ONAL
Mb

32.
32,

163.
163.

20.
115.
135.

100.
100.

160.
160.

0.
0.

120.
120.

0.
10.
0.
10.

50.
50.

37.
37.


CONSTRUCTION
NO.

0
0

2
2

0
5
'5

3
3

0
0

1
1

0
0

1
0
2
3

0
0

0
0
MM

0.
0.

450.
450.

0.
2236.
2236.

660.
660.

0.
0.

550.
550.

0.
0,

400.
0.
730.
1130.

0.
0.

0.
0.
                                    206
PEDCO ENVIRONMENTAL

-------
                                    TABLE 6
                         SUMMARY OF FGU SYSTEMS BY VENDOR

                                          	STATUS	
                                 TOTAL    OPERATIONAL  CONSTRUCTION

MANUFACTURER/PROCESS          NO.     MW   NO.     Mta   NO.     MW
                                61 19760.    30  6459.    31 13309.
                                                             207                                PEDCO ENVIRONMENTAL

-------
20d                                PEOCO ENVIRONMENTAL

-------
                    TABLE  7




SUMMARY OF I\IEW AND RETROFIT FGD SYSTEMS BY PROCESS
                         209                PEDCO-ENVIRONHENTAL

-------
210                                PEDCO  ENVIRONMENTAL

-------
                                                   TABLE 7
                                 SUMMARY OF NEW AND KETKOFJT FGD SYSTEMS BY PROCESS
                                         MW CAPACITY(NO. OF PLANTS)
            PROCESS

LIME SCRUBBING
LIME/ALKALINE FLYAsH SCRUBBING
 (PROCESS NOT SELECTED)

LIME/LIMESTONE SCRUBBING
 (PROCESS NOT SELECTED)

LIMESTONE SCRUBBING
  SUBTOTAL - LIME/LIMESTONE
AQUEOUS CARBONATE SCRUBBING
DOUBLE ALKALI SCRUBBING
MAGNESIUM OXIDE SCRUBBING
NOT SELECTED
REGENERABLE NOT SELECTED
SODIUM CARBONATE SCRUBBING
THOROUGHBRED 101
WELLMAN LORD/ALLIED CHEMICAL
          TOTALS
  LIME/LIMESTONE X OF TOTAL MU
NLU OR
OPERATIONAL
CONSTRUCTION
RETROFIT

N
R
I N
R
N
R
N
R
N
R
N
R
N
R
N
R
N
R
N
R
N
R
N
R
N
R
N
R
1 N
R
NO.
1
7
2
0
0
2
5
7
6.
16.
0
0
0
1
0
1
0
0
0
0
1
2
0
1
0
0
9.
21.


MU
635
1407
720
0
0
20
2067
860
3622.
2287.
0
0
0
32
0
120
0
0
0
0
125
250
0
23
0
0
3747.
2712.
97
64
NO. MM
7 3575
1 163
1 450
0 0
0 0
0 0
17 7146
1 550
2*. 11171.
2. 733.
0 0
0 0
1 575
0 0
0 0
0 0
0 0
0 0
0 0
0 0
0 0
0 0
0 0
0 0
1 375
2 455
27.12121.
4. 1166.
92
62
CONTRACT
AWARDED
NO.
6
0
2
0
0
0
6
1
16.
1.
0
0
1
1
0
0
0
0
0
0
1
0
0
0
0
0
18.
2.


MU
3150
0
1400
0
0
0
3970
425
6520.
425.
0
0
250
277
0
0
0
0
0
0
509
0
0
0
0
0
9279.
702.
92
61
LETTER OF REQUESTING/
INTENT
NO.
0
0
0
0
0
0
0
0
0.
0.
0
0
0
0
0
1
0
0
0
0
1
0
0
0
0
0
1.
1.


MU
0
0
0
0
0
0
0
0
0.
o.
0
0
0
0
0
240
0
0
0
0
125
0
0
0
0
0
125.
240.
0
0
EVAL. BIOS
NO.
0
0
0
0
1
0
0
0
1.
0.
0
0
0
0
0
0
3
0
0
0
0
0
0
0
0
0
4.
0.


MU
0
0
0
0
527
0
0
0
527.
0.
0
0
0
0
0
0
1600
0
0
0
0
0
0
0
0
0
2327.
0.
23
0
CONSIDERING
TUTAL NO,
OF PLANTS
FGD SYSTEM
NO.
0
2
0
0
2
2
3
0
5.
4.
0
1
0
0
0
2
16
6
2
1
0
0
0
0
0
0
23.
14.


MU
0
660
0
0
900
1410
1260
0
2160.
2070.
0
100
0
0
0
486
7920
2320
1000
650
0
0
0
0
0
0
11100.
5626.
20
37
NO.
14
10
5
0
3
4
33
9
55.
23.
0
1
2
2
0
4
19
6
2
1
3
2
0
1
1
2
82.
42.


MW
7560
2250
2570
0
1427
1430
14463
1835
26020.
5515.
0
100
825
309
0
846
9720
2320
1000
650
759
250
0
23
375
455
38699.
10466.
67
S3
                                                               211
PEDCO ENVIRONMENTAL

-------
212                                PEDCO ENVIRONMENTAL

-------
                           TABLE  6




SUMMARY OF OPERATING FGD SYSTEMS BY PROCESS AND GENERATING UNITS
                                213                PEOCO-ENVIRONMENTAL

-------
21t                                PCOCO ENVIRONMENTAL

-------
                      TABLE a
           SUMMARY OP OPERATING FGD SYSTEMS BY
           PROCESS AND GENERATING UNITS AS OF 12/76
  PROCESS/GENERATING UNITS
                    FGO/MU  STARTUP  EXPERIENCE(MO.)
        DOUBLE ALKALI SCRUBBING

CHEVROLET PARMA 1 2 3 S 4
                                     32.
                              3-74
                          33

                          33
        LIME SCRUBBING

BHUCE MANSFIELD NO, 1
CANE HUN NO 4
ELRAMA POWER STATION
FOUR CORNERS NO. 5A
GREEN RIVER   UNITS i AND 2
PADDYS RUN NO 6
PHILLIPS POWER STATION
RICKENBACKER
                      835
                      178
                      510
                      160
                       64
                       65
                      410
                       20
        4-76
        8-76
       10-75
        2-76
        9-75
        4-73
        7-73
        3-76
                                   2242.
                    8
                    4
                   14
                   10
                   15
                   44
                   41
                    9

                  145
        LIME/ALKALINE FLYASH SCRUBBING
COLSTRIP NO 1
COLSTRIP NO 2
                      360
                      360
                                    720.
       10-75
        7-76
                   14
                    5

                   19
        LIME/LIMESTONE SCRUBBING
SHAUNEE N0.10A
SHAWNEE N0.10B
                       10
                       1U
                                     20.
        4-72
        4-72
                   56
                   56

                  112
        LIMESTONE SCRUBBING
HAWTHORN NO 3
HAWTHORN NO 4
LAWRENCE NO 4
LAWRENCE NO 5
CHOLLA NO 1
DUCK CREEK NO.
LA CY6NE NO 1
1A
14 U
100
125
400
115
100
620
11-72
 8-72
12-68
11-71
10-73
 9-76
 2-73
49
52
96
61
36
 3
46
                                                            215
                                                                               PEDCO ENVIRONMENTAL

-------
                      TABLE 6
           SUMMARY OF OPERATING FGO SYSTEMS BY
           PROCESS AND GENERATING UNITS AS OF 12/76
  PROCESS/GENERATING UNITS         FGD/MW  STARTUP  EXPERIENCED.)
SHERBURNE COUNTY STATION NO.l        710     3-76               9
ST. CLAIR NO 6                       163     5-76               7
STOCK ISLAND PLANT                    37    10-72              50
VALMONT NO. 5                         50    10-7
-------
                           TABLE  9



SUMMARY OF SLUDGE DISPOSAL PRACTICES FOR OPERATIONAL F6D SYSTEMS
                                217                PEDCO-ENVIRONMENTAL

-------
218                                 PEDCO ENVIRONMENTAL.

-------
                            TABLE 9
        SUMMARY OF SLUDGE DISPOSAL PRACTICES FOR OPERATIONAL  F6D  SYSTEMS  AS OF   12/76
PROCESS/GENERATING UNIT
—SLUuGE—      --SLUUGL--      —POND—       —POND-
STABILIZED    UNSTABILI2ED        LINED          UNLINED
      DOUBLE ALKALI SCRUBBING

CHEVROLET PARMA 1 2 3 & 4

      TOTAL
                        32

                        32.
                 0.
                32

                32.
      LIME SCRUBBING

BRUCE MANSFIELD NO. 1
CANE RUN NO 4
ELRAMA POWER STATION
GREEN RIVER   UNITS 1 AND 2
PADDYS RUN NO 6
PHILLIPS POWER STATION
RICKENBACKER

      TOTAL
       835
       178
       510
        64

       410
      1997.
65

20

85.
20

20.
               835
               178
               510
                64
                65
               410
                                                                                         2062.
      LIME/ALKALINE FLYA&H SCRUBBING
COLSTRIP NO 1
COLSTRIP NO 2

      TOTAL
                       360
                       360

                       720,
                                                                             0.
                               360
                               360

                               720.
      LIMESTONE SCRUBBING

HAWTHORN NO 3
HAWTHORN NO 4
LAWRENCE NO 4
LAWRENCE NO 5
CHOLLA NO 1
DUCK CREEK NO. 1A
LA CYGNE NO 1
SHERBURNE COUNTY STATION NO.l
ST. CLAIR NO 6
STOCK ISLAND PLANT
VALMONT NO. 5
WILL COUNTY NO 1

     • TOTAL
       167

       167.
                       140
                       100
                       125
                       400
                       115
                       100
                       820
                       710
                       163
                        37
                        50
                                                          2760.
               100

               710
               163

                50
               167

              1190.
               140
               100
               125
               400
               115

               620
                37
              1737.
                                                          219
                                                         PCOCO  ENVIRONMENTAL

-------
                            TABLE 9
        SUMMARY OF SLUDGE DISPOSAL PRACTICES FOR OPERATIONAL FGO SYSTEMS AS OF  12/76
PROCESS/GENERATING UNIT             —SLUDGE—      —SLUDGE—      —POND—      	POND-
                                    STABILIZED    UNSTABILI2ED        LINED          UNLINED
SODIUM CARBONATE SCRUBBING
REID GARDNER NO 1
REID GARDNER NO 2
REID GARDNER NO 3

125
125
125

125
125
125
      TOTAL                                  0.            375.              0.            375.


      THOROUGHBRED 101

SCHOLZ NOS. IB * 28                                         23              23

      TOTAL                                  0.             23.             23.              0.
                                                          220                                PEOCO ENVIRONMENTAL

-------
                      TABLE 10



SUMMARY OF FGD SYSTEMS BY PROCESS ANJ REGULATORY CLASS
                           221                PEDCO-ENVIRONMENTAL

-------
222                                 PEOCO EHV1RONKEN-IM.

-------
                                                   TABLL 10
                                 SUMMARY OF FGO SYSTEMS BY PROCESS AND REGULATORY CLASS

                                         MU CAPACITY(NO. OF PLANTS)
            PROCESS

LIME SCRUBBING
LIME/ALKALINE FLYASH SCRUBBING
 (PROCESS NOT SELECTED)
LIME/LIMESTONE SCRUBBING
  (PROCESS NOT SELECTED)
LIMESTONE  SCRUBBING
   SUBTOTAL - LIME/LIMESTONE
REGULATORY OPERATIONAL
CLASS
NO.
A 0
B 4
C 3
0 0
E 1
ENG A 1
B 0
C 1
D 0
E 0
A 0
B 0
C 2
D 0
E 0
A I
B 4
C 4
D 2
E 1
A 2.
B 8.
C 10.
D 2.
E 2.
CONSTRUCTION
CONTRACT
AWARDED
MU
0
1915
307
0
2U
360
0
360
0
0
0
0
20
0
0
100
1065
1167
525
50
460.
2980.
187*.
525.
70.
NO.
5
2
1
0
0
0
1
0
0
G
0
0
0
0
0
11
6
1
0
0
16.
9.
2.
0.
0.
MU
2340
1235
163
0
0
0
450
0
0
0
0
0
0
0
0
4456
2690
550
0
0
6796.
4375.
733.
0.
0.
NO.
4
2
0
0
0
2
0
0
0
0
0
0
0
0
0
3
4
1
0
1
9.
6.
1.
0.
1.
MU
1915
1235
0
0
0
1400
0
0
0
0
0
0
0
0
0
1770
1800
425
0
too
5065.
3035.
425.
0.
400.
LETTER OF REQUESTING/
INTENT
NO.
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
C
0
0
0
0.
0.
0.
0.
0.
MU
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0.
0.
0.
0.
0.
CVAL.
NO.
0
0
0
0
0
0
0
0
0
0
1
0
0
0
0
0
0
0
0
0
1.
0.
0.
0.
0.
BIDS
MU
0
0
0
0
0
0
0
0
0
0
527
0
0
0
0
0
0
0
0
0
527.
0.
0.
0.
0.
CONSIDERING
TOTAL NU.
OF PLANTS
FGD SYSTEM
NO.
0
0
2
0
0
0
0
0
0
0
0
2
0
0
2
2
1
0
0
0
2.
3.
2.
0.
z.
MM
0
0
660
0
0
0
0
0
0
0
0
900
0
0
1410
930
350
0
0
0
930.
1250.
660.
0.
1410.
NO.
9
a
6
0
1
3
1
1
0
0
1
2
2
0
2
17
15
6
2
2
30.
26.
15.
2.
5.
MU
4255
4385
1150
0
20
1760
450
360
0
0
527
900
20
0
1410
7256
5905
2162
525
45Q
13798.
11640.
3692.
525.
IfldO.
   A.   BOILER CONSTRUCTED SUBJECT  TO  FEDERAL NSPS
   B.   BOILER SUBJECT TO STATE  STANDARD  THAT IS MORE STRINGENT THAN THE FEDERAL NSPS
   c.   BOILER SUBJECT TO STATE  STANDARD  THAT is EQUAL TO OK LESS STRINGENT THAN NSPS
   D.   OTHER
   E.   REGULATORY CLASS UNKNOWN
                                                               223
PEDCO ENVIRONMENTAL

-------
                                                   TABLE: 10
                                 SUMMARY OF FGD SYSTEMS BY PROCESS AND REGULATORY CLASS

                                         MU CAPACITY(NO. OF PLANTS)
            PROCESS

AQUEOUS CARBONATE SCRUBBING
DOUBLE ALKALI SCRUBBING
MAGNESIUM OXIDE SCRUBBING
NOT SELECTED
REGENERABLE NOT SELECTED
REGULATORY OPERATIONAL
CLASS

A
B
C
0
E
A
B
C
0
E
A
B
C
D
E
A
B
C
D
E
A
B
C
D
E
NO.
0
0
0
0
0
0
1
0
0
0
0
1
0
0
0
0
0
0
0
0
o'
0
0
0
0
MW
0
0
0
0
0
0
32
0
0
0
0
120
0
0
0
0
0
0
0
0
0
0
0
0
0
CONSTRUCTION
NO.
0
0
0
0
0
1
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
MW
0
0
0
0
G
575
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
C
CONTRACT
AWARDED
NO.
0
0
0
0
0
1
0
1
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
MW
0
0
0
0
0
250
0
277
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
LETTER OF REQUESTING/
INTENT EVAL. BIDS
NO.
0
0
0
0
0
0
0
0
0
0
0
1
0
0
0
0
0
0
0
0
0
0
0
0
0
MW
0
0
0
0
0
0
0
0
0
0
0
2
-------
                                                   TABLE 10
                                 SUMMARY OF FGD SYSTEMS BY PROCESS MO REGULATORY CLASS


                                         M* CAPACITY(NO. OF PLANTS)
            PROCESS


SODIUM CARBONATE SCRUBBING
THOROUGHBRED 101
UELLMAN LORD/ALLIED CHEMICAL
           TOTALS
   LIME/STONE  X OF  TOTAL  HW
REGULATORY OPERATIONAL
CLASS

A
B
C
D
E
A
B
C
D
E
A
B
C
D
E
A
B
C
D
E
A
B
C
0
E
NO.
0
3
0
0
0
0
0
1
0
0
0
0
0
0
0
2.
13.
11.
2.
2.
100
as
99
100
100
MW
0
375
0
0
0
0
0
23
0
0
0
0
0
0
0
460.
3507.
1697.
525.
70.





CONSTRUCTION
NO. MW
0
0
0
0
0
0
0
0
0
0
0
2
1
0
0
17
11
3
0
0





0
0
0
0
0
0
0
0
0
0
0
715
115
0
0
. 7371.
. 5090.
. a<*8.
o.
0.
92
86
86
0
0
CONTRACT
AWARDED
NO.
0
1
0
0
0
0
0
0
0
0
0
0
0
0
C
10.
7.
2.
0.
1.





MW
0
509
0
0
0
0
0
0
0
0
0
0
0
0
0
5335.
35
-------
226                                PEDCO ENVIRONMENTAL

-------
            TABLE 11




SUMMARY OF OPERATIONAL FGD SYSTEMS
                 227                 PEDCO-ENVIRONMENTAL

-------
22a                                PEDCO ENVIRONMENTAL

-------
                      TABLE 11
            SUMMARY OF OPERATIONAL FGD SYSTEMS AS OF 12/76
       UTILITY COMPANY
        POWER STATION
 NEM OR   SIZE OF FGO  PROCESS/VENDOR
RETROFIT   UNIT (HW)
 FUEL CHARACTERISTICS
MO/YR
ARIZONA PUBLIC SERVICE
FOUR CORNERS NO. 5A

ARIZONA PUBLIC SERVICE
CHOLLA NO 1

CENTRAL ILLINOIS LIGHT CO.
DUCK CREEK NO. 1A

COMMONWEALTH EDISON
WILL COUNTY NO 1

DETROIT EDISON
ST. CLAIR NO 6

DUOUESNE LIGHT
PHILLIPS POWER STATION

OUUUESNL LIGHT
ELRAMA POWER STATION

GENERAL MOTORS
CHEVROLET PARMA  1  2 3 &  t

GULF POWER  CO.
SCHOLZ NOS.  IB  & 2B

KANSAS CITY  POWER  & LIGHT
HAWTHORN NO  3

KANSAS CITY  POWER  & LIGHT
HAWTHORN NO  4

KANSAS CITY  POWER  & LIGHT
LA  CYGNL NO 1

KANSAS POWER &  LIGHT
LAWRENCE NO 1

KANSAS POWER &  LIGHT
LAWKENCE NO 5

KENTUCKY UTILITIES
GREEN RIVER   UNITS 1 AND 2
R
R
N
R
R
R
R
R
R
R
K
N
R
N
R
160
115
100
167
163
mo
510
32
23
140
100
820
125
too
6H
                      SO. CALIFORNIA EDISON
                      LIME SCRUBBING

                      RESEARCH COTTRELL
                      LIMESTONE SCRUBBING

                      RILEY STOKER / ENVIRONEERING
                      LIMLSTONE SCRUBBING

                      BABCOCK & WILCOX
                      LIMESTONE SCRUBBING

                      PEABODY ENGINEERING
                      LIMESTONE SCRUBBING

                      CHEMICO
                      LIME SCRUBBING

                      CHEMICO
                      LIME SCRUBBING

                      KOCH/GENERAL MOTORS
                      DOUBLE ALKALI SCRUBBING

                      CHIYODA INTERNATIONAL
                      THOROUGHBRED 101

                      COMBUSTION ENGINEERING
                      LIMESTONE INJECTION &WET SCRUB

                      COMBUSTION ENGINEERING
                      LIMESTONE INJECTION iWET SCRUB

                      BABCOCK & WILCOX
                      LIMESTONE SCRUBBING

                      COMBUSTION ENGINEERING
                      LIMESTONE INJECTION SWET SCRUB

                      COMBUSTION ENGINEERING
                      LIMESTONE INJECTION &WET SCRUB

                      AMERICAN AIR FILTER
                      LIME SCRUBBING
COAL  0.7 PERCENT SULFUR         2/76
COAL   0.4t-l PERCENT SULFUR    10/73
COAL 2.5 - 3.0 PERCENT SULFUR    9/76
COAL <».0 PERCENT SULFUR          2/72
COAL  3.7 PERCENT SULFUR         5/76
COAL   i.o- 2.8 PERCENT SULFUR   7/73
COAL  i.o - 2.8 PERCENT SULFUR  10/75
COAL   2.5 PERCENT SULFUR        3/71
COAL 5.0 PERCENT SULFUR (MAX)    3/75
COAL   0.6- 3.0 PERCENT SULFUR  11/72
COAL   0.6- 3.0 PERCENT SULFUR   8/72
COAL 5.0 PERCENT SULFUR          2/73
COAL 0.5 PERCENT SULFUR         12/68
COAL 0.5 PERCENT SULFUR         11/71
COAL  3.8 PERCENT SULFUR         9/75
                                                              229
                                                                 PEOCO ENVIRONMENTAL

-------
                      TABLE 11
            SUMMARY OF OPERATIONAL FGO SYSTEMS AS OF ia/76
       UTILITY COMPANY
        POWER STATION
 KEY WEST UTILITY BOARD
 STOCK  ISLAND PLANT

 LOUISVILLE GAS & ELECTRIC
 PADDYS RUN NO 6

 LOUISVILLE GAS £ ELECTRIC
 CANE RUN NO 4

 MONTANA POWER CO.
 COLSTRIP NO 1

 MONTANA POUER CO.
 COLSTRIP NO 2

 NEVADA POWER
 REID GARDNER NO 1

 NEVADA POWER
 REID GARDNER NO Z

 NEVADA POWER
 REID GARDNER NO 3

 NORTHERN STATES POWER CO.
 SHERBURNE COUNTY STATION NO.l

 PENNSYLVANIA POWER CO.
 BRUCE  MANSFIELD NO. i

 PHILADELPHIA ELECTRIC CO.
.EDDYSTONE NO 1A

 PUBLIC SERVICE CO OF COLORADO
 VALMONT NO. 5

 RICKENBACKER AFB
 RICKENBACKER

 TENNESSEE VALLEY AUTHORITY
 SHAUNEE NO.IOB

 TENNESSEE VALLEY AUTHORITY
 SHAWNEE NO.10A
NEW OR
RETROFIT
N
R
R
N
N
R
R
N
N
N
R
R
R
R
R
SIZE OF FGO
UNIT (MW)
37
65
178
360
360
125
125
125
710
835
120
50
20
10
10
 PROCESS/VENDOR
ZURN AIR SYSTEMS
LIMESTONE SCRUBBING

COMBUSTION ENGINEERING
LIME SCRUBBING

AMERICAN AIR FILTER
LIME SCRUBBING

ACL/COMBUSTION E«UIP ASSOCIATE
LIME/ALKALINE FLYASH SCRUBBING

ADL/COMBUSTION EUUlP ASSOCIATE
LIME/ALKALINE FLYASH SCRUBBING

AOL/COMBUSTION EQUIP ASSOCIATE
SODIUM CARBONATE SCRUBBING

ADL/COMBUSTION EQUIP ASSOCIATE
SODIUM CARBONATE SCRUBBING

ADL/COMBUSTION EQUIP ASSOCIATE
SODIUM CARBONATE SCRUBBING

COMBUSTION ENGINEERING
LIMESTONE SCRUBBING

CHEMICO
LIME SCRUBBING

UNITED ENGINEERS / PECO
MAGNESIUM OXIDE SCRUBBING

UOP / PUB SERVICE OF COLORADO
LIMESTONE SCRUBBING

RESEARCH COTTRELL
LIME SCRUBBING

CHEMICO
LIME/LIMESTONE SCRUBBING

UNIVERSAL OIL PRODUCTS
LIME/LIMESTONE SCRUBBING
 FUEL CHARACTERISTICS           MO/YR
OIL    2.4 PERCENT SULFUR       10/72
COAL  3.5-4.0 PERCENT SULFUR     4/73
COAL 3*5 - 4.0 PERCENT SULFUR    6/76
COAL   0.8 PERCENT SULFUR       10/75
COAL   0.8 PERCENT SULFUR        7/76
COAL   0.5- ItO PERCENT SULFUR   4/74
COAL   o.s- i.o PERCENT SULFUR   4/74
COAL   o.s- i.o PERCENT SULFUR   7/76
COAL 0.8 PERCENT SULFUR
COAL 4.7 PERCENT SULFUR
COAL   2.5 PERCENT SULFUR
COAL  0.72 PERCENT SULFUR
COAL 3.6 PERCENT SULFUR
COAL 2.9 PERCENT SULFUR
COAL 2.9 PERCENT SULFUR
 3/76


 4/76


 9/75


10/74


 3/76


 4/72


 4/72
                                                              230
                                           PEDCO ENVIRONMENTAL

-------
                TABLE \
-------
232                                PCDCO ENVIRONMENTAL

-------
                      TABLE 12
            SUMMARY OF FGO SYSTEMS UNDER CONSTRUCTION AS OF 12/76
       UTILITY COMPANY
        POWER STATION
 NEW OR   SIZE OF FGD  PROCESS/VENDOR
RETROFIT   UNIT 
-------
                      TABLE 12
            SUMMARY OF FGO SYSTEMS UNDER CONSTRUCTION AS OF 12/76
       UTILITY COMPANY
        POWER STATION
 NEW OR   SIZE. OF F&O  PROCESS/VENDOR
RETROFIT   UNIT 
-------
                      TABLE 12
            SUMMARY OF FGD SYSTEMS UNDER CONSTRUCTION AS OF 12/76
       UTILITY COMPANY
        POWER STATION
 NEW OR
RETROFIT
SIZE OF FGD
 UNIT (MM)
PROCESS/VENDOR
FUEL CHARACTERISTICS
MO/YR
UTAH POWER & LIGHT CO.
HUNTIfcGTON NO.l
                      CHEMICO
                      LIME SCRUBBING
                                            COAL  0.5 PERCENT SULFUR
                                                                6/77
                                                              235
                                                                 PEOCO ENVIRONMENTAL

-------
>PEOCO  ENVIRONMENTAL

-------
          TABLE 13




SUMMARY OF PLANNED FGD SYSTEMS
               237                 PEDCO-ENVIRONMENTAL

-------
238                                PEUCO ENVIRONMENTAL

-------
                   TABLE 13
            SUMMARY OF PLANNED FGD SYSTEMS AS OF 12/76
       UTILITY COMPANY
        POWER STATION
            CONTRACTS AWARDED

BASIN ELECTRIC POuER COOP
MISSOURI BASIN NO 2

COLUMBUS ft SOUTHERN OHIO ELEC.
COUESVILLE NO 6

PENNSYLVANIA POUER CO.
BRUCE MANSFIELD NO. 3

BASIN ELECTRIC POwER COOP
MISSOURI BASIN NO 1

PACIFIC POUER AND LIGHT CO*
JIM BKIOGER NO. 4

MONTANA POWER CO.
COLSTRIP NO.4

MONTANA POWER CO.
COLSTRIP NO.3

LOUISVILLE GAS & ELECTRIC
CANE RUN NO 6

BRAZOS ELECTRIC POWER  COOP
ATACOSA MCMULLCN NO. 1

COMMONWEALTH EDISON
PCWERTON NO. 51

LOUISVILLE GAS & ELECTRIC
MILL CREEK NO 4

TEXAS UTILITIES CO.
MARTIN LAKE NO. 4

UTAH POWER & LIGHT CO.
EMERY NO.l

SOUTHERN INDIANA GAS&ELECTRIC
A.B. BROWN NO.l

SOUTHERN ILLINOIS POWER COOP
SOUTHERN ILLINOIS POWER PT. 4
NEW OR
RETROFIT
N
N
N
N
N
N
N
R
N
R
N
N
N
N
N
SIZE OF FGD
UNIT (MW)
550
400
635
550
509
700
700
277
400
425
425
793
400
250
184
 VENDOR/PROCESS
 FUEL CHARACTERISTICS
MO/YR
RESEARCH COTTRELL
LIMESTONE SCRUBBING

UNIVERSAL OIL PRODUCTS
LIME SCRUBBING

PULLMAN KELLOGG
LIME SCRUBBING

RESEARCH COTTRELL
LIMESTONE SCRUBBING

UNIVERSAL OIL PRODUCTS
SODIUM CARBONATE SCRUBBING

ADL/COMBUSTION EQUIP ASSOCIATE
LIME/ALKALINE FLYASH SCRUBBING

ADL/COMBUSTION EQUIP ASSOCIATE
LIME/ALKALINE FLYASH SCRUBBING

AUL/COMBUSTION EQUIP ASSOCIATE
DOUBLE ALKALI SCRUBBING

BABCOCK & WILCOX
LIMESTONE SCRUBBING

UNIVERSAL OIL PRODUCTS
LIMESTONE SCRUBBING

AMERICAN AIR FILTER
LIME SCRUBBING

RESEARCH COTTRELL
LIMESTONE SCRUBBING

CHEMICO
LIME SCRUBBING

FMC CORPORATION
DOUBLE ALKALI SCRUBBING

BABCOCK £ WILCOX
LIMESTONE SCRUBBING
COAL
COAL  4.5 - 4.9 PERCENT SULFUR
COAL 4.7 PERCENT SULFUR
LIGNITE 0.8 PERCENT SULFUR
COAL 0.56 PERCENT SULFUR
-------
                   TABLE; is
            SUMMARY OF PLANNED FGD SYSTEMS AS OF ia/?t,
       UTILITY COMPANY
        POWER STATION
 NEW OR   SIZE OF FGD  VENDOR/PKOCESS
RETROFIT   UNIT 
FUEL CHARACTERISTICS
MO/YR
UNITED POWER ASSOCIATION
COAL CREEK NO. 2

UNITED POWER ASSOCIATION
COAL CREEK NO. 1

SALT RIVER PROJECT
CORONADO NO.2

SALT RIVER PROJECT
CORONADO NO.l

TEXAS UTILITIES Co.
MARTIN LAKE NO. 3
            LETTER OF INTENT SIGNED
NEVADA POWER
REID GARDNER NO 4

PHILADELPHIA ELECTRIC CO.
EDOYSTONE NO IB
            REQUESTING/EVALUATING BIOS

MINNESOTA POWER AND LIGHT co.
CLAY BOSWELL STATION NO.4

PU3LIC SERVICE OF INDIANA
GIBSON NO. 4

PUBLIC SERVICE OF INDIANA
GIBSON NO. 3

WISCONSIN POWER & LIGHT CO.
COLUMBIA NO. 2
            CONSIDERING FGD SYSTEM
NEVADA POWER
WARNER VALLEY STATION NO. 1

NEVADA POWER
HARRY ALLEN STATION NO. 2
N
N
N
N
N
N
R
OS
N
N
N
N
N
N
545
545
350
350
793
125
240
500
650
fa50
527
250
500
COMBUSTION ENGINEERING
LIME SCRUBBING
COMBUSTION ENGINEERING
LIME SCRUBBING
PULLMAN KELLOGG
LIMESTONE SCRUBBING
PULLMAN KELLOGG
LIMESTONE SCRUBBING
RESEARCH COTTRELL
LIMESTONE SCRUBBING-
AOL/COMBUSTION EQUIP ASSOCIATE
SODIUM CARBONATE SCRUBBING
UNITED ENGINEERS / PECO
MAGNESIUM OXIDE SCRUBBING
NOT SELECTED
NOT SELECTED
NOT SELECTED
NOT SELECTED
NOT SELECTED
NOT SELECTED
NOT SELECTED
LIME/LIMESTONE SCRUBBING
NOT SELECTED
NOT SELECTED
NOT SELECTED
NOT SELECTED
LIGNITE
LIGNITE
COAL 1.
COAL 1.
COAL 1.
COAL
COAL 2.
COAL 0.
COAL 3.
COAL 3.
COAL 0.
COAL
COAL
- 0.63 PERCENT SULFUR
- 0.63 PERCENT SULFUR
0 PERCENT SULFUR (MAX)
0 PERCENT SULFUR (MAX)
0 PERCENT SULFUR
0-5- itO PERCENT SULFUR
5 PERCENT SULFUR
8 PERCENT SULFUR
3 PERCENT SULFUR
3 PERCENT SULFUR
8 PERCENT SULFUR


11/79
11/78
4/80
4/79
12/78
O/ 0
6/80
0/80
0/79
0/78
1/80
6/82
6/84
                                                              240
                                                                 PEOCO ENVIRONMENTAL

-------
                   TABLE 13
            SUMMARY OF PLANNED FGD SYSTEMS AS OF 12/76
       UTILITY COMPANY
        POWER STATION
 NEW OR   SI2E OF FGD  VENDOR/PROCESS
RETROFIT   UNIT (HW)
                                                                                       FUEL CHARACTERISTICS
                                                                                      MO/YR
NEVADA POWER
HARRY ALLEN STATION NO. 3

BASIN ELECTRIC POWER COOP
MISSOURI BASIN NO 3

BASIN ELECTRIC POwER COOP
ANTELOPE VALLEY NO. 1

BASIN ELECTRIC POWER COOP
ANTELOPE VALLEY NO. 2

LOUISVILLE  GAS &  ELECTRIC
MILL CREEK  NO 1

LOUISVILLE  GAS &  ELECTRIC
MILL CREEK  NO 2

PHILADELPHIA ELECTRIC  CO.
CROMBY

CENTRAL ILLINOIS  LIGHT CO.
DUCK  CREEK  NO.2

CINCINNATI  GAS  &  ELECTRIC CO.
EAST  BEND NO 2

COLORADO UTE ELECTRICAL ASSN.
CRAIG STATION NO.l

 COLORADO UTE ELECTRICAL ASSN.
 CRAIG STATION NO.2

 COLUMBUS & SOUTHERN OHIO ELEC.
 POSTON NO.  f>

 INDIANAPOLIS POWER £ LIGHT CO.
 PETERSBURG NO f

 COLUMBUS & SOUTHERN OHIO ELEC.
 POSTON NO. 5

 EASTERN KENTUCKY POWER COOP
 SPURLOCK GENERATING PLANT NO.2

 NEVADA POWER
 HARRY ALLEN STATION NO. 1
N
N
N
N
R
R
R
N
N
N
N
N
N
N
N
N
500
550
450
450
330
330
150
400
(,00
450
450
375
530
375
500
500
NOT SELECTED
NOT SELECTED
NOT SELECTED
NOT SELECTED
NOT SELECTED
NOT SELECTED
NOT SELECTED
NOT SELECTED
NOT SELECTED
LIME SCRUBBING
NOT SELECTED
LIME SCRUBBING
UNITED ENGINEERS / PECO
MAGNESIUM OXIDE SCRUBBING
NOT SELECTED
LIMESTONE SCRUBBING
NOT SELECTED
NOT SELECTED
NOT SELECTED
LIME/LIMESTONE SCRUBBING
NOT SELECTED
LIME/LIMESTONE SCRUBBING
MOT SELECTED
NOT SELECTED
NOT SELECTED
LIMESTONE SCRUBBING
NOT SELECTED
NOT SELECTED
NOT SELECTED
NOT SELECTED
NOT SELECTED
NOT SELECTED
                                                                                      COAL                             6/85
                                                      COAL                             6/83
                                                      LIGNITE 1.0 PERCENT SULFUR       0/81
                                                      LIGNITE 1.0 PERCENT SULFUR       0/84
                                                      COAL   3.5- t.o PERCENT SULFUR   1/82
                                                      COAL   3.5- 4*0 PERCENT SULFUR   1/81
                                                      COAL   2-4 PERCENT SULFUR        6/80
                                                      COAL 2.5-3.0 PERCENT SULFUR      1/82
                                                      COAL                             1/81
                                                      COAL 0.45 PERCENT SULFUR         3/79
                                                      COAL 0.45 PERCENT SULFUR         3/79
                                                       COAL 2.5 PERCENT SULFUR          0/83
                                                       COAL  3.5 PERCENT SULFUR          4/62
                                                       COAL 2.5 PERCENT SULFUR          0/81
                                                       COAL                            3/80
                                                       COAL                            6/83
                                                               241
                                                                                                  PEOCO ENVIRONMENTAL

-------
                   TABLE 13
            SUMMARY OF PLANNED F6D SYSTEMS AS OF l2/7fa
       UTILITY COMPANY
        POWER STATION
 NEW OR   SIZE OF FGD  VENDOR/PROCESS
RETROFIT   UNIT (MM)
FUEL CHARACTERISTICS
MO/YR
NEVADA POWER
WARNER VALLEY STATION NO. 2
PHILADELPHIA ELECTRIC CO.
EDDYSTONE NO. 2
OTTER TAIL POWER COMPANY
COYOTE STATION NO.l
ARIZONA PUBLIC SERVICE
FOUR CORNERS NO. 4
NORTHERN STATES POWER co.
SHERBURNE COUNTY STATION NO.3
NORTHERN STATES POWER CO.
SHERBURNE COUNTY STATION NO.«*
ARIZONA PUBLIC SERVICE
FOUR CORNERS NO. 58
NORTHERN INDIANA PUB SERVICE
BAILLY NO. 7
NORTHERN INDIANA PUB SERVICE
BAILLY NO. 8
NIAGARA MOHAWK POnER COOP.
CHARLES R. HUNTLEY NO. 6
NEW ENGLAND ELEC SYSTEM
BRAYTON POINT NO.3
NEVADA POWER
HARRY ALLEN STATION NO. if
SOUTHERN CALIFORNIA EDISON
MOHAVE NO IB
SOUTHERN CALIFORNIA EDISON
MOHAVE NO. 2
SALT RIVER PROJECT
CORONADO NO.3
POTOMAC ELECTRIC & POWER
OICKERSON NO.l
N
R
N
R
N
N
R
R
R
R
R
N
R
R
N
R
250
336
400
755
660
860
595
190
too
100
650
500
620
790
350
190
NOT SELECTED
NOT SELECTED
UNITED ENGINEERS / PECO
MAGNESIUM OXIDE SCRUBBING
NOT SELECTED
NOT SELECTED
NOT SELECTED
NOT SELECTED
NOT SELECTED
NOT SELECTED
NOT SELECTED
NOT SELECTED
NOT SELECTED
NOT SELECTED
NOT SELECTED
NOT SELECTED
NOT SELECTED
NOT SELECTED
ATOMICS INTERNATIONAL
AUUEOUS CARBONATE SCRUBBING
NOT SELECTED
REGEIMERABLE NOT SELECTED
NOT SELECTED
NOT SELECTED
NOT SELECTED
LIME/LIMESTONE SCRUBBING
NOT SELECTED
LIME/LIMESTONE SCRUBBING
NOT SELECTED
LIMESTONE SCRUBBING
CHEMICO
NOT SELECTED
                                                      COAL                             6/83
                                                      COAL 2.if PERCENT SULFUR          6/80
                                                      LIGNITE 0.9 PERCENT,SULFUR       0/81
                                                      COAL  0.7 - 0.758 SULFUR (AVG)   O/ 0
                                                      COAL 0.8 PERCENT SULFUR
                                                      COAL 0.6 PERCENT SULFUR
                                5/81
                                5/83
                                                      COAL  0.7 - 0.75S SULFUR (AVG)   O/ 0
                                                      COAL 3 PERCENT SULFUR            O/ 0
                                                      COAL 3 PERCENT SULFUR            O/ 0
                                                      COAL 2.5-
-------
                   TABLE 13
            SUMMARY OF PLANNED FGO SYSTEMS AS OF 12/76

       UTILITY COMPANY           NEW OR   SIZE OF FGD  VENDOR/PROCESS                  FUEL CHARACTERISTICS           MO/YR
        POWER STATION           RETROFIT   UNIT (MU)


POTOMAC ELECTRIC & POWER            R        190      CHEMICO                         COAL                             0/76
DICKERSON NO.2                                        NOT SELECTED

PUBLIC SERVICE CO OF NEW HEX.       N        500      NOT SELECTED                    COAL 0*8 PERCENT SULFUR          5/81
SAN JUAN NO. t                                        REGENERABLE NOT SELECTED

PUBLIC SERVICE CO OF NEW MEX.       N        500      NOT SELECTED                    COAL 0*6 PERCENT SULFUR          5/81
SAN JUAN NO. 3                                        REGENERABLE NOT SELECTED
                                                              2
-------
2H<*                                 PEOCO ENVIRONMENTAL

-------
                       TABLE 1H




SUMMARY LIST OF FGD SYSTEMS IN THE EARLY PLANNING STAGES
                                               PEDCO-ENVIRONMENTAL

-------
PEOCO ENVIRONMENTAL

-------
                                         TABLE  IH
               SUMMARY  LIST  OF  FGD  SYSTEMS  IN  THE EARLY PLANNING STAGES
 F6D STATUS  REPORT  12/76

 1.0. NUMBER AND  COMPANY  NAME
   UNIT NAME
       LOCATION
START UP DATE   STATUS
REG
CLASS
    1  GENERAL  PUBLIC  UTILITIES
    2  GENERAL  PUBLIC  UTILITIES
    3  GULF  POWER  CO.
    n  GULF  POWER  co.
    5  GULF  POWER  co,
    6  KENTUCKY UTILITIES
    7  POTOMAC  ELECTRIC & POWER
    8  POTOMAC  ELECTRIC & POWER
    9  POWER AUTHORITY OF NEW YORK
   10  SALT  RIVER  PROJECT
   11  SALT  RIVER  PROJECT
   12  SALT  RIVER  PROJECT
   13  SPRINGFIELD WATER LIGHT  POWER
   l«f  TEXAS POWER AND LIGHT CO.
   15  TEXAS POWER AND LIGHT CO.
   16  VIRGINIA ELECTRIC AND POWER co
COHO NO.l
SEWARU NO.7
CRIST NO. 4 AND NO. 5
CKIST NO. 6 AND NO. 7
LANSING SMITH NO, 1 AND NO.
GHENT NO. 2
CHALK POINT NO. H
DICKERSON NO H
ARTHUR KILL
NAVAJO NO 1
NAVAJO NO 2
NAVAJO NO 3
DALLMAN NO 3
TWIN OAKS NO. 1
TWIN OAKS NO. 2
HT, STORM
ERIE PENNSYLVANIA                   5-87       7
SEWARO PENNSYLVANIA                 5-8t       7
PtNSACOLA FLORIDA                   0-78       7
PENSACOLA FLORIDA                   0-80       7
PANAMA CITY FLORIDA                 0-80       7
GHENT KENTUCKY                      0-0       7
PRINCE GEORGE COUNTY MARYLAND       0-80       7
DICKERSON MARYLAND                  5-82       7
STATEN ISLAND NEW YORK              9-82       7
PAGE ARIZONA                        0-0       7
PAGE ARIZONA                        0-0       7
PAGE ARIZONA                        0-0       7
SPRINGFIELD ILLINOIS                6-79       7
ROBERTSON COUNTY  TEXAS             8-80       7
ROBERTSON COUNTY  TEXAS             9-61       7
MT, STORM WEST VIRGINIA             0-0       7
                            A
                            A
                            B
                            B
                            B
                            E
                            D
                            D
                            B
                            D
                            D
                            D
                            A
                            A
                            A
                            C
7. CONSIDERING FGD SYSTEM AS WELL AS ALTERNATIVE METHODS

A.  BOILER CONSTRUCTED SUBJECT TO FEDERAL NSPS
D.  BOILER SUBJECT TO STATE STANDARD THAT IS MORE STRINGENT THAN THE FEDERAL NSPS
C.  BOILER SUBJECT TO STATE STANDARD THAT IS EQUAL TO OR LESS STRINGENT THAN NSPS
D.  OTHER
C.  REGULATORY CLASS UNKNOWN
                                                             2*7
                                                           PEDCO ENVIRONMENTAL

-------
PEDCO ENVIRONMENTAL

-------
                    TABLE 15




STATUS OF FGD SYSTEMS IN THE EAKLY PLANNING STAGES
                                            PEDCO-ENVIRONMENTAL

-------
250                                PEOCO ENVIRONMENTAL

-------
 COMPANY

 POWER STATION
                     TABLE 15
STATUS OF FGD SYSTEMS IN THE EARLY PLANNING STAGES DURING

                                 CURRENT MONTH
                        12/76
1.0. NUMBER    1
GENERAL PUBLIC UTILITIES
COHO NO.l
  800  MW - NEW
COAL
NOT SELECTED
NOT SELECTED
STARTUP   5/87
              STARTUP DATE CHANGED TO 5/67 FOR BOTH BOILER AND FGD SYSTEM.  LIME, LIME-
              STONE SCRUBBING, AND COAL OESULFURIZATION ARE THE PRIMARY PROCESSES BEING
              CONSIDERED.  NO DECISION HAS BEEN MADE YET.
I.D. NUMBER    2
GENERAL PUBLIC UTILITIES
SEWARD NO.7
  800  MW - NEW
COAL
NOT SELECTED
NOT SELECTED
STARTUP   5/8H
              STARTUP DATE CHANGED TO 5/8
-------
 COMPANY

 POWER STATION
                     TABLE 15
STATUS OF FGD SYSTEMS IN THE EARLY PLANNING STAGES DURING  12/76

                                 CURRENT MONTH
I.D. NUMBER    6
KENTUCKY UTILITIES
GHENT NO. 2
  510  MW - NEW
COAL   3.0 PERCENT SULFUR
NOT SELECTED
LIME SCRUBBING
STARTUP   O/ 0
              THIS NEW COAL-FIkED POWER BOILER WAS SUPPLIED BY COMBUSTION
              ENGINEERING-AND IS SCHEDULED TO COMMENCE COMMERCIAL
              OPERATION IN JANUARY 1977.  THE UTILITY ALSO HAS AN EXISTING
              510-MW COAL-FIRED UNIT INSTALLED AT THIS STATION AND IS
              PRESENTLY EVALUATING PLANS TO INSTALL A SCRUBBER ON ONE
              OF THESE TWO UNITS.
I.D. NUMBER    7
POTOMAC ELECTRIC & POWER
CHALK POINT NO. i»
  630  MW - NEW
OIL
NOT SELECTED
NOT SELECTED
STARTUP   0/80
              AWAITING PERFORMANCE RESULTS FROM MGO UNIT ON DICKERSON NO. 3 (MONTGOMERY
              COUNTY).  UNIT WILL HAVE PEABODY-LURGI 2-STAGE VENTURI SCRUBBERS FOR PAR-
              TICULATE CONTROL.  COMPANY MAY ELECT NOT TO INSTALL FGD SYSTEM IF USE OF
              LOW SULFUR OIL IS CONTINUED.
I.D. NUMBER    8
POTOMAC ELECTRIC & POWER
DICKERSON NO 
-------
 COMPANY
 POWER STATION
                     TABLE 15
STATUS OF FGO SYSTEMS IN THE EARLY PLANNING STAGES DURING

                                 CURKENT MONTH
12/76
I.D. NUMBER   11
SALT RIVLR PROJECT
NAVAJO NO 2
  750  MW - RETROFIT
COAL   0.45 PERCENT SULFUR
NOT SELECTED
LIME/LIMESTONE SCRUBBING
STARTUP   O/ 0
              THE. UTILITY IS PRESENTLY INVESTIGATING THE USE OF LOW SULFUR COAL AND
              DESULFURIZATION PROCESSES. A DEFINITIVE DECISION WILL BE MADE PENDING
              COMPLETION OF THE SRP/EPA STUDY. NO SPECIFIC STARTUP DATE HAS YET BEEN
              SPECIFIED.
1.0. NUMbER   12
SALT RIVER PROJECT
NAVAJO NO 3
  750  MW - RETROFIT
COAL   0.<»5 PERCENT SULFUR
NOT SELECTED
LIME/LIMESTONE SCRUBBING
STARTUP   O/ 0
              THE UTILITY IS PRESENTLY INVESTIGATING THE USE OF LOW SULFUR COAL AND
              DESULFUR1ZATION PROCESSES. A DEFINITIVE DECISION WILL BE MADE PENDING
              COMPLETION OF THE SRP/EPA STUDY. NO SPECIFIC STARTUP DATE HAS YET BEEN
              SPECIFIED.
I.D. NUMBER   13
SPRINGFIELD WATER LIGHT  POWER
DALLMAN NO 3
  190  MW - NEW
COAL   3.0- «».3 PERCENT SULFUR
NOT SELECTED
NOT SELECTED
STARTUP   6/79
              FGD SYSTEM IS UNDER CONSIDERATION WITH BOTH REGENERABLE AND LlMESToNE
              SCRUBBING BEING CONSIDERED.  BECAUSE OF SPACE LIMITATIONS A REGENERABLE:
              SYSTEM IS THE LIKELY CHOICE.  THE COMPANY IS ALSO CONSIDERING COMPLIANCE
              THROUGH BURNING OF LOW SULFUR WESTERN COAL.
I.D. NUMBER   l
-------
                                             TABLE 15
 COMPANY                STATUS OF FGD SYSTEMS IN THE EARLY PLANNING STAGES  DURING   13/76

 POWER STATION                                           CURRENT NONTH
• .____*_««.* — *_* — *»**•• —— — ^••••••w**_»~~~-.« —** — — •••*•» — **-_*<_• — •*.»**-.•..<•» — •**••••_«•_•*__._*•._•_*••_•••••*•_..•*.
1.0, NUMBER   16                      THE UTILITY IS PRESENTLY CONSIDERENG  BOTH  DESULFURIZATION AND THE USE OF
VIRGINIA ELECTRIC AND POWER CO        LOW SULFUR COAL. A DESULFURIZATION SYSTEM  WOULD  TREAT 69 PERCENT OF THE
hT. STORh                             FLOE GAS FROM THREE BOILERS. CONSTRUCTION  AND STARTUP DATES ARE CON-
 Il«f7  MW - RETROFIT                  SIDERED INDEFINITE AT THIS TIME.
COAL
NOT SELECTED
NOT SELECTED
STARTUP   O/ 0
                                                                2St                                 PCDCO ENVIRONMENTAL

-------
                               APPENDIX A




FbD SYSTEM OPERATIONS THAT HAVE BEEN TERMINATED OR SHUT DOWN INDEFINITELY
                                 A"]                    PEDCO-ENVIRONMENTAL

-------
A-2

-------
            APPENDIX A
TERMINATED OPERATIONAL FGD SYSTEMS
 IDENTIFICATION NO.
 UTILITY NAME
 UNIT NAME
 UNIT LOCATION
 UNIT RATING
 FUEL CHARACTERISTICS
 FGD VENDOR
 PROCESS
 NEW OR RETROFIT
 START UP DATE
 FGO STATUS
 EFFICIENCY,
  PARTICULARS

  S02

 WATER HAKE UP

 SLUDGE DISPOSAL

 UNIT COST
 OPERATIONAL
  EXPERIENCE
   1
 BOSTON EDISON
 MYSTIC NO 6
 EVLRETT MASSACHUSETTS
  ISO  MW
 OIL    2.5 PERCENT SULFUR
 CHEMICO
 MAGNLSIUH OXIDE SCRUBBING
 RETROFIT
  H/72

 TERMINATED

 50 PERCENT

 90 PERCENT
 ACID PLANT REGENERATION
S32/KW CAPITAL + CALCINATION
 AVERAGE FGD SYSTEM AVAILABILITY FACTORS - APRIL 72 TO MAY 73* 17X.
 JUNE 73 TO DEC. 73, 48X.  JAN. 74 TO JUNE 74. 60S.  JUNE 74, 80X.
 THE F6D SYSTEM HAS BEEN SHUT DOWN INDEFINITELY SINCE JUNE 74.
                                                             A-3
                                                                                                      PEDCo ENVIRONMENTAL

-------
                                                           BACKGROUND INFORMATION
                                                                     ON
                                                    THE MYSTIC POWER STATION, UNIT  NO.  6


     THE MAGNESIUM OXIDE-BASED FPO SYSTEM INSTALLED AT THE MYSTIC POWER  STATION  OF  THE  BOSTON  EDISON COMPANY  CONSISTS OF A CHEMICO-DESIGNED SINGLE-
STAGE VENTURI SCRUBBER MODULE.  THE MODULE IS CONSTRUCTED OF CARBON STEEL  LINED  KITH A  SPRAY-APPLIED POLYESTER MATERIAL.  TOTAL FLUE GAS CAPACITY OF
THE SYSTEM IS 440,000 ACFM AT 300°F.  MAXIMUM DESIGN SULFUR DIOXIDE CONCENTRATION AND REMOVAL  EFFICIENCY  IS 1500 PPM AND 90 PERCENT RESPECTIVELY.
     THIS EXPERIMENTAL MAGNESIUM OXIDE SCRUBBING UNIT IS RETROFITTED ON  A  155-MW, OIL-FIRED  STEAM-GENERATING  BOILER MANUFACTURED BY COMBUSTION
ENGINEERING.  THIS BOILER FIRES NO. 6 RESIDUAL FUEL OIL WITH THE FOLLOWING AVERAGE  CHARACTERISTICS:  HEAT CONTENT OF 149,000 BTU/GAL; ASH CONTENT OF
0.07 PERCENT; AND A SULFUR CONTENT OF 2.0 PERCENT.   THE UNIT'S HEAT RATE IS APPROXIMATELY  9500 BTU/NET  KWH.
     SIMULTANEOUS REMOVAL OF SULFUR DIOXIDE AND PARTICULATES OCCURS IN THE VENTURI  SCRUBBER  MODULE.  DESIGN REMOVAL EFFICIENCIES ARE 90 PERCENT AND
55 PERCENT RESPECTIVELY.  SULFUR DIOXIDE REMOVAL FROM THE FLUE GAS OCCURS  BY WET SCRUBBING WITH MAGNESIUM OXIDE SLURRY.  THE SULFUR DIOXIDE IS
CAPTURED AND CONVERTED TO MAGNESIUM SULFITE IN THE  VENTURI.  THIS PRODUCT  SLURRY IS THEN  FILTERED AND DRIED.  THE DRY MATERIAL IS CALCINED AT HIGH
TEMPERATURES TO DRIVE OFF THE SULFUR DIOXIDE AND REGENERATE MAGNESIUM OXIDE. THE SULFUR  DIOXIDE STREAM IS PROCESSED IN A SULFURIC ACID PLANT TO MAKE
98 PERCENT GRADE OF SULFURIC ACID.  A SCHEMATIC FLOW DIAGRAM OF THE SCRUBBING AND REGENERATION FACILITIES IS  PRESENTED IN FIGURE 22.APPENDIX C.
     THE UTILITY AND THE EPA PROVIDED THE MAJOR PORTION OF THE FUNDING FOR THIS  REGENERABLE  DEMONSTRATION PROJECT.  EACH PARTY CONTRIBUTED APPROXIMATELY
$4.5 MM TO THE PROJECT.  BOSTON EDISON'S INVESTMENT HAS BEEN SPENT PRIMARILY ON  CONSTRUCTION AND OPERATION OF THE SCRUBBER AND RELATED EQUIPMENT
AT THE MYSTIC STATION.  EPA'S INVESTMENT WAS PROVIDED PRIMARILY FOR THE  REGENERATION FACILITIES AT ESSEX  CHEMICAL'S SULFURIC ACID PLANT IN RUMFORD,
RHODE ISLAND.  THE SYSTEM SUPPLIER ALSO UNDERWROTE  PART OF THE COSTS FOR FUTURE  PROCESS DEVELOPMENT.
PROBLEMS AND SOLUTIONS
     FROM THE INITIAL START-UP IN APRIL 1972 UNTIL  MAY 1973 THE SCRUBBER OPERATED INTERMITTENTLY BECAUSE  OF MECHANICAL DIFFICULTIES.  THE MAJOR PROBLEM,
ENTAILING DESIGN AND OPERATION OF THE MAGNESIUM SULFITE CRYSTAL DRYER, APPARENTLY HAS  BEEN RESOLVED BY  REDESIGN AND FUEL CHANGE.  PROBLEMS WITH THE
STACK AND PUMP OCCURRED DURING USE OF REGENERATED MAGNESIUM OXIDE.  OVERHEATING  OF  THE  SLURRY  DURING ACTIVATION OF THE STEAM FREEZE PROTECTION SYSTEM
CAUSED FORMATION OF SCALE IN THE MgO SLURRY PIPING.  IN 1974, SYSTEM OPERATION WAS  LIMITED BY  BOILER AVAILABILITY.  SINCE FEBRUARY 1974 AVAILABILITY
OF THE BOILER HAS BEEN INCREASED.  THE SYSTEM HAS BEEN SHUT DOWN INDEFINITELY SINCE JUNE  1974, WHEN EPA FUNDS FOR THE CALCINING PORTION OF THIS OPERATION
WERE EXHAUSTED.
     AVAILABILITY FACTORS AND COMMENTS CONCERNING THE OPERATION OF THIS  SYSTEM SINCE STARTUP ARE PRESENTED IN THE FOLLOWING TABLE.

                                                                            A-4
                                                                                                                          PEDCo ENVIRONMENTAL

-------
                                                           FGD SYSTEM AVAILABILITY
                                                              MYSTIC UNIT NO.  6

           Boiler     Scrubber
          Operation  Operation
Month       (hr)       (hr)      Operabnity (X)                                          Comments
Apr. 72                             17                 The module operated Intermittently because of mechanical  difficulties.   A major problem con-
   to                                                  cerned the operation of the magnesium sulfite crystals dryer.
May  73
Jun. 73     592        402          68                 The longest period of continuous operation, 7.5 days, occurred during June  and July.
Jul. 73     575        351          61
Aug. 73        Boiler shutdown                         The boiler was down for the annual overhaul.  System availability decreased during  the last
Sep. 73     637        243         38                 quarter of the year because of heavy erosion/corrosion In the liquor recirculation  pumps  and
Oct. 73     627        377         60                 centrifuge.
Nov. 73     629        162         26
Dec. 73     658          86         13
Jan. 74      555        152         28                 System availability was limited by boiler-related problems that caused frequent shutdowns in
Feb. 74      541        138         25                 January and February.
Har. 74     408       353         87
Apr. 74      585       471         81                 Two 7-day continuous operation periods occurred during the month.
May 74      488       280         57                 The 57 percent operability index value for the month was  due to a 2-weeks outage  of the acid
Jun.  74      559       288         80                 plant rather than to FGO system failure.  Demonstration program was completed and FGD system
                                                       was shut down.  EPA funding of MgS03 calcination has expired.   There are no definite plans for
                                                       restarting of this unit.  Major problem areas encountered during the operation of this proto-
                                                       type unit Included trihydrate instead of hexahydrate sulfite crystal formation, dust problems
                                                       in the dryer, lack of stack gas reheat causing condensation in the stack, louver  damper
                                                       problems, erosion of pumps, piping, and centrifuge, and minor ancillary equipment failures.


                                                                          A-5
                                                                                                                         PEDCo ENVIRONMENTAL

-------
                     APPENDIX A
  TERMINATED OPERATIONAL FGD SYSTEMS
IDENTIFICATION NO.
UTILITY NAME
UNIT NAME
UNIT LOCATION
UNIT RATING
DAIRYLAND POWER COOP

ALMA STATION

ALMA WISCONSIN

  60 MW
FUEL CHARACTERISTICS  COAL   3.0- 3.5 PERCENT SULFUR
FGD VENDOR
PROCESS

NEW OR RETROFIT

START UP DATE

FGD STATUS

EFFICIENCY.
 PARTICULATES
FOSTER WHEELER

LIME INJECTION

RETROFIT

 6/71

TERMINATED
 S02
25 PERCENT
WATER MAKE UP
SLUDGE DISPOSAL
UNIT COST
OPERATIONAL
 EXPERIENCE
THIS EXPERIMENTAL WET LIME FURNACE INJECTION SYSTEM HAS BEEN OPERATIONAL
SINCE 1971 FOR PERIODS UP TO 30 DAYS.  IN AUGUST 1974 THE UNIT WAS TESTED
FOR TWO DAYS USING WESTERN LOW SULFUR COAL.  THE TEST SHOWED ABOUT SOX
S02 REMOVAL EFFICIENCY. BUT PRECIPITATOR PERFORMANCE WAS ADVERSELY
AFFECTED.  THE FGD PROJECT HAS BEEN SHUT DOWN INDEFINITELY SINCE
AUGUST 1974. AND THERE ARE NO PLANS FOR FUTURE OPERATION.
                                                              A-6
                                                                                                    PEDCo ENVIRONMENTAL

-------
        APPENDIX A
TERMINATED OPERATIONAL F6D SYSTEMS
luLMIFlCATlOH  NO.

UTILITY l-HKE.

UMIT NAfiL

UfilT LOCATION

UMIT KwTliMG

FUEL CHARACTERISTICS

FGli VENDOR

PROCESS

NEW OK RETROFIT

START UP  DATE

FGD STATUS

EFFICIENCY.
  PftRTICULATES
GULF POWER CO.

SCHOL2 NO. 1A

CHATTAHOOCHEE  FLORIDA

  20 Mta

COAL   3.0 PERCENT SULFUR

AOL/COnBUSTION EuUIP  ASSOCIATE

DOUBLE ALKALI SCKUBBIUG

RETKOFIT
 TERMINATED


 99.7  PERCENT
  S02
                       9b PERCENT
 WATLK f.AKL UP
        DISPOSAL
 CLOSED LOOP
 DESTABILIZED SLUUSE DISPOSED IN LINED POND
 UNIT COST
 OPERATIONAL
  EXPERIENCE
 REFLK  TO  THE BACKGROUND INFORMATION SECTION IN APPENDIX A OF THIS REPORT.
 THIS PHOTOTYPE  SCRUBBING SYSTEM UAS INITIALLY PLACED Ih SERVICE
 1973 AND  WAS OPERATIONAL A TOTAL 
-------
                                                           BACKGROUND INFORMATION



                                                                     ON



                                                        SCHOLZ NO.  1A - DOUBLE ALKALI







     THE SCHOLZ STEAM POWER PLANT OF GULF POWER COMPANY IS LOCATED  IN CHATTAHOOCHEE, FLORIDA.   UNIT  NO.  1  IS A  COAL-FIRED STEAK BOILER DESIGNED AND



INSTALLED BY BABCOCK AND WILCOX IN 195*.  THIS UNIT IS NOMINALLY RATED AT 40  MW AND IS  CAPABLE  OF  47.5 MW  MAXIMUM CAPACITY.  THIS UNIT FIRES VARIOUS



TYPES OF COAL FOR TEST PURPOSES.  THE AVERAGE CHARACTERISTICS OF THE COAL BURNED IN THIS  UNIT DURING THE FGD DEMONSTRATION PROGRAM ARE:  HEAT CONTENT



OF 12,400 BTU/LB; MAXIMUM SULFUR CONTENT OF 5 PERCENT; ASH CONTENT  OF 14 PERCENT;  AND A MAXIMUM CHLORIDE CONTENT OF 0.15 PERCENT.



     A 20-MW PROTOTYPE DUAL ALKALI SYSTEM WAS JOINTLY DEVELOPED, DESIGNED, AND INSTALLED  BY  COMBUSTION EQUIPMENT ASSOCIATES AND ARTHUR D. LITTLE.  THE



PROTOTYPE SYSTEM AT THE SCHOLZ STEAM PLANT IS INSTALLED ON THE NO.  1 BOILER.  THE  SYSTEM  IS  DESIGNED TO  HANDLE  APPROXIMATELY 50 PERCENT OF THE FLUE GAS



FROM THE BOILER.  THE BOILER HAS BEEN RETROFITTED WITH A SECTIONALIZED, HIGH-EFFICIENCY ESP  INSTALLED UPSTREAM  OF THE FGD SYSTEM AND CAPABLE OF 99.7



PERCENT PARTICULATE REMOVAL.  THE ESP CAN BE SELECTIVELY DE-ENERGIZED FOR STUDY OF PARTICULATE  IMPACT ON THE FGD OPERATION.



     THE PROTOTYPE UNIT INCORPORATES A HIGH DEGREE OF FLEXIBILITY FOR GENERATION OF DESIGN AND  OPERATING INFORMATION FOR A WIDE VARIETY OF APPLICATIONS.



ALTHOUGH THE BASIC MODE OF SYSTEM OPERATION IS DUAL ALKALI WITH LIME REGENERATION, THE  SYSTEM WAS  DESIGNED TO ACCOMMODATE LIMESTONE REGENERATION



AND LIME/LIMESTONE REGENERATION.  THE SYSTEM CONSISTS OF A VENTURI  SCRUBBER AND AN ABSORPTION TOWER, WITH  AN ADDITIONAL STORAGE SILO FOR LIMESTONE. A



MIX TANK, AND OTHER ASSORTED TANKS, PUMPS, CONTROLLERS, PIPING, AND A LINED DISPOSAL POND.



     THE PROTOTYPE SYSTEM WAS COMPLETED AND PUT IN OPERATION BY CEA/ADL IN EARLY FEBRUARY 1975.   IN  MID-MAY AN  EPA DUAL ALKALI TEST PROGRAM WAS



INITIATED BY SOUTHERN SERVICES, CEA, AND ADL.  THE SYSTEM WAS OPERATIONAL THROUGH  EARLY JANUARY 1976, WHEN THE  BOILER WAS SHUT DOWN FOR A SCHEDULED



OVERHAUL.  THE BOILER AND PROTOTYPE SYSTEM WERE PLACED BACK IN SERVICE IN EARLY MARCH 1976.  THE SYSTEM  HAS OPERATED CONTINOUSLY DURING THIS



PERIOD ON A HIGH SULFUR COAL (3.5 TO 4.5 PERCENT) APPLICATION, TREATING FLUE  GAS WITH SULFUR DIOXIDE CONCENTRATIONS IN THE 2000 TO 2500 PPM RANGE.  IN



ADDITION, SYSTEM WAS TESTED OUT ON FLUE GAS OF VARYING PARTICULATE  LOADING TO DETERMINE THE  IMPACT OF FLY  ASH OF SYSTEM OPERATIONS.  THE PROTOTYPE



PROGRAM WAS SUCCESSFULLY CONCLUDED ON JULY 3, 1976 AT 6 A.M.  RESULTS OF THE  PROGRAM ARE  BEING  PREPARED  FOR PUBLICATION.  THIS PROCESS IS NOW SCHEDULED



FOR FULL SCALE DEMONSTRATION APPLICATION AT LOUISVILLE GAS AND ELECTRIC'S CANE RUN NO.  6  UNIT.



     THE PERFORMANCE OF THE SCHOLZ PROTOTYPE UNIT AND COMMENTS ARE  LISTED BELOW  IN THE  PERFORMANCE TABLE.   A PROCESS FLOW DIAGRAM OF THE SCHOLZ PROTOTYPE



FGD UNIT IS PROVIDED IN FIGURE 23 OF APPENDIX C.
                                                                           A-8                                                PEDCo ENVIRONMENTAL

-------
                                        SCHOLZ 1A - DOUBLE ALKALI
Unit Operating Hours
Period
Feb. 75
Har. 75
Apr. 75
May 75
Jun. 75
Jul. 75
Aug. 75
Sep. 75
Oct. 75
Nov. 75
Dec. 75
Total
hours
672
744
720
744
720
744
744
720
744
720
744
Boiler
459
507
604
598
720
683
744
577
559
620
732
F6D system
454
485
336
375
720
221
0
254
55S
560
732
FGD system
operabillty
99
96
56
63
100
32
0
44
100
90
100
Performance (1
utilization
68
65
47
50
100
30
0
35
75
78
98
                                                                                       Comnents
                                                         Unit was placed in operation February 8, 1975, and operated until  July
                                                         18 when it was shut down for 2 months modifications, repairs, and
                                                         replacement of parts.  The system was unavailable to the boiler for
                                                         a 491-hour period because of adjustments and modifications required for
                                                         the formal EPA test program in mid-May.
                                                         The system was shut down from mid-July to mid-September for mechanical
                                                         overhaul involving replacement parts for valves that had failed.

                                                         The system was put back in operation on September 16, 1975.  From mid-
                                                         September to mid-October the air preheater was repaired and boiler
                                                         operation adjusted to reduce oxygen levels in the flue gas to the  5 to
                                                         6 percent range.  The system operated approximately 800 hours during
                                                         this period.
                                                         The system ran continuously for the remainder of the test period through
                                                         January 2, 1976.  S02 levels during this period ranged from 800 to
                                                         1700 ppm.  The system operated in the concentrated mode throughout
                                                         the remainder of the test period.  In the period from mid-September to
                                                         January 2, 1976, the system operated about 2100 hours, with an
                                                         operabillty factor of 97 percent.
                                                   A-9
                                                                                                 PEDCo  ENVIRONMENTAL

-------
                                                   SCHOLZ  1A  - DOUBLE ALKALI (continued)
  Period
Jan. 76
Feb. 76
Apr. 76
Nay  76
Jun. 76
Total
hours
744
696
Mar. 76    744
720
744
720
                       Unit Operating Hours
Boiler    FGD system
           742
 642
 735
             445
616
651
 656
641
             FGD system   Performance  (X)
            operabiHty    utilization
                60
96
89
               60
86
88
93
89
                    Comments
The FGD system and boiler underwent a scheduled overhaul  during  the
report period.  System restart is scheduled for mid-March 1976,  to con-
tinue till June.  During this operating period high-sulfur coal
(3.5-4.0 percent) will be burned to allow evaluation of system per-
formance on high-sulfur coal.
The system was put back In service on March 12, 1976.  The total number
of operating hours for the month of March was 445 hours.   This trans-
lates into a 94% operability factor since the March 12 restart.
Some minor mechanical problems in the form of agitator shaft and
control value failures were encountered during the report period.
Since the system restart on March 12, high sulfur coal has been
burned in the boiler (3.5 to 4.5 percent sulfur), resulting in the
SO- inlet concentration levels in the 2000 to 2500 ppm range.
During the last phase of operation, the system was treating flue gas
of varying particulate loads.  The upstream ESP was selectively
de-energized, both partially and totally.  No major upsets in the
process chemistry occurred.  Boiler load variation ranged from 30 to
100 percent.  The prototype program at the plant was successfully
conducted on July 2.  ADL is currently completing data acquisition and
analysis.
                                                                         A-10
                                                                                                                        PEDCo ENVIRONMENTAL

-------
                                                    SCHOLZ 1A - DOUBLE ALKALI  (continued)

                       Unit Operating Hours
           Total                               F6D system   Performance (X)
  Period   hours     Boiler    F6D system     operablHty    utilization                                     Comments
Jul. 76    744         54*         54            100*                          The  prototype test program was successfully concluded on July 3, 1976.

                                                                               *Note:   The  boiler hours,  system operation hours, and the corresponding
                                                                                       performance value  calculated Includes system operation up to
                                                                                       the  scheduled shutdown, which occurred on July 3,  6:00 A.M.,
                                                                                       1976.
                                                                         A - 1 1                                    PEDCo ENVIRONMENTAL

-------
                    APPENDIX A
           TERMINATED OPERATIONAL FGD  SYSTEMS
IDENTIFICATION NO.
UTILITY NAME
UNIT MAME
UNIT LOCATION
UNIT RATING
FUEL CHARACTERISTICS
FGD VENDOR
PROCESS
NEW OR RETROFIT
START UP DATE
FGO STATUS
EFFICIENCY!
 PARTICULATES

 S02

UATER MAKE UP
GULF POWER CO.
SCHOLZ NO. 2A
CHATTAHOOCHEE  FLORIDA
  20 HW
COAL   3.0 PERCENT  SULFUR
FOSTER WHEELER
ACTIVATED CARBON
RETROFIT
 3/76
TERMINATED

99.7 PERCENT

7
-------
                                                                BACKGROUND INFORMATION



                                                                          ON



                                                              SCKOLZ NO.  2A - FWBF SYSTEM







     IN JANUARY 1973, THE SOUTHERN SERVICES COMPANY OF GULF POWER AWARDED A CONTRACT TO THE FOSTER WHEELER CORPORATION TO  BUILD A 20 MW PROTOTYPE DRY



ADSORPTION SYSTEM FOR FLUE GAS DESULFURIZATION.  CONSTRUCTION ON THE FOSTER WHEELER PROCESS STARTED FEBRUARY 15,  1974, AT  THE  SCHOLZ STEAM POWER



PLANT IN CHATTACHOOCHEE, FLA.  CONSTRUCTION WAS COMPLETED AND A TESTING PROGRAM WAS INITIATED IN MAY 1975.



     THE SYSTEM AT THE SCHOLZ PLANT CONSISTS OF A 20-MW ADSORBER SECTION AND A 47.5-MW REGENERATION AND REDUCTION SECTION.  THE 20 MW ADSORBER  IS



DESIGNED TO ACCEPT HALF OF THE MAXIMUM FLUE GAS FLOW FROM UNIT NO. 2.  THE COAL-FIRED BOILER IS RATED AT 40 MW (NOMINAL);  IT FIRES COAL WITH AN AVERAGE



HEATING VALUE OF 12,400 BTU/LB.  MAXIMUM ASH AND SULFUR CONTENTS ARE 14 AND 5 PERCENT, RESPECTIVELY.



     THE PURPOSE OF THE ADSORPTION SECTION OF THE FWBF DRY REMOVAL SYSTEM IS TO REMOVE SULFUR DIOXIDE, NITROGEN OXIDES,  AND PARTICULAR FROM THE FLUE



GAS WITH ACTIVATED CHAR, CONVERTING THE CAPTURED POLLUTANTS TO SULFURIC ACID.  THE REGENERATION SECTION PROVIDES  CONTINUOUS ON-SITE REGENERATION OF



THE CHAR, WHICH HAS BEEN LOADED WITH SULFUR DIOXIDE IN THE FORM OF SULFURIC ACID.  THE CHAR IS REGENERATED AND A  LOW-VOLUME, SULFUR DIOXIDE-RICH



OFF-GAS STREAM IS FED FORWARD TO THE RESOX REACTOR, WHICH REDUCES THE SULFUR DIOXIDE STREAM TO GASEOUS ELEMENTAL  SULFUR  THAT IS COLLECTED AND STORED IN



AN INSULATED TANK.



     THE DEMONSTRATION UNIT HAS TWO ROWS OF MODULES, EACH ROW CONSISTING OF SIX MODULES.  THE ADSORPTION SECTION  IS A TWO-STAGE DESIGN CONSISTING



OF VERTICAL COLUMNS OF PARALLEL LOUVER BEDS WHICH SUPPORT AND CONTAIN THE ACTIVATED CHARCOAL.  SULFUR DIOXIDE, OXYGEN, WATER VAPOR, AND NITROGEN OXIDES



ARE ADSORBED BY THE CHAR PELLETS FROM THE CROSS-FLOWING FLUE GAS AT 250 TO 300°F.  THE SULFUR DIOXIDE THEN REACTS WITH OXYGEN  AND WATER TO FORM SUL-



FURIC ACID WHICH IS FIRMLY RETAINED IN THE INTERIOR PORE SYSTEM OF THE CHAR PELLETS.  THE CHAR IS THEN REGENERATED IN THE  REGENERATOR VESSEL BY HEATING



TO 1200°F, DRIVING OFF THE ENTRAINED GASES, AND REDUCING SULFURIC ACID TO SULFUR DIOXIDE.  THE SULFUR DIOXIDE-RICH GAS IS  THEN PASSED THROUGH A VESSEL



CONTAINING CRUSHED COAL, RESULTING IN REDUCTION TO GASEOUS ELEMENTAL SULFUR AND CARBON DIOXIDE.  THIS LATTER PROCESS IS  CARRIED OUT AT 1200° TO 1500°F.



A SCHEMATIC OF THE PROCESS COMPONENTS FOR THE FW-BF DRY ADSORPTION IS PRESENTED IN FIGURE 24 OF APPENDIX C.



     THE INITIAL SHAKEDOWN ON FLUE GAS BEGAN AUGUST 11, 1975, AND PROCEEDED CONTINUOUSLY FOR 10 DAYS.  THE REGENERATION  SECTION WAS OPERATIONAL ABOUT



60 PERCENT OF THE TIME.  HOWEVER, THE REDUCTION SECTION HAS NOT YET BEEN INTEGRATED INTO SYSTEM OPERATION.  SULFUR DIOXIDE REMOVAL WAS WELL ABOVE



EXPECTATIONS AND PRESSURE DROP ACROSS THE ADSORBER HAS WELL BELOW DESIGN LEVELS.  THE SYSTEM WAS SHUT DOWN FOR CORRECTION  OF SEVERAL OPERATING  PROBLEMS,
                                                                                                                     PEDCo ENVIRONMENTAL




                                                                            A-13

-------
SCHOLZ NO. 2A - FWBF SYSTEM (Continued)
EQUIPMENT MODIFICATIONS, AND EVALUATION OF THE INTIAL OPERATING DATA.   OPERATION WAS RESUMED IN  OCTOBER 1975, WHEN TWO CONSECUTIVE RUNS WERE  CONDUCTED
WITH THE REDUCTION PORTION OF THE SYSTEM PROCESSING FRONT-END OFF-GAS  AT FULL OPERATING TEMPERATURES.   A PROGRAM OF MODIFICATION WAS COMPLETED  ON THIS
SYSTEM IN EARLY JANUARY 1976.  REPRODUCTION OF FLUE GAS INTO THE INTEGRATED SYSTEM COMMENCED IN  FEBRUARY 1976.  OPERATIONS THROUGH A FINAL  4-MONTH
TEST PROGRAM WERE PREMATURELY TERMINATED ON MAY 2, 1976.
                                                                         A -1 4                                    pEDCo ENVIRONMENTAL

-------
                          FHBF SYSTEM OPERATING HISTORY

Period                                                         Comments
May 75                             Completion of construction was followed by a 3-month commissioning period during which
Jun. 75                            various pieces of equipment were operated individually and then in combinations to
Jul. 75                            simulate subsystem operation.  Subsystem operations were integrated into section
Aug. 75                            operations and flue gas was passed through the adsorber and regenerator for a 10-day
                                   period beginning August 11.  RESOX construction was incomplete at this time.
Oct. 75                            Two consecutive runs were conducted on the RESOX portion of the system on front-end
                                   process off-gas at full operating temperatures.  This operational period lasted 5
                                   days.
Nov. 5                             A program of modifications on the system began in late August 1975 and continued
Dec. 75                            through January 1976, with the exception of the 5-day RESOX operation in October.
Jan. 75                            Modifications were completed and pre-startup testing was conducted in late January
                                   and early February.  A 3-day continuous dry run was successfully completed.
Feb. 76                            All materials-handling loops and RESOX loops were operated at full operating
                                   temperatures and pressures.  Reintroduction of flue gas into the system commenced,
                                   and a 4-month formal test program conducted by Southern Services and Foster Wheeler
                                   is now in progress.
Mar. 76                            Three operational periods were logged by the prototype system during the report
Apr. 76                            months.  During these runs the adsorption and regeneration sections performed
                                   adequately.  The RESOX section operated intermittently because of plugging problems
                                   1n the sulfur condenser.  Also, the front end of the system was taken down at one
                                   point due to frequent high temperature excursions.  This problem was corrected by
                                   modifying system operating procedures.  Currently, work 1s proceeding on the
                                   solution of the sulfur condenser problem.

                                            A-1 5                                     PEDCo  ENVIRONMENTAL

-------
                    FMBF SYSTEM OPERATING HISTORY (Continued)

Period                                                         Comments
May 76                             The FW-BF unit completed an operational  period in  early May which  had  commenced on
                                   April 26.  The system was taken down at  this  point for the following reasons:
                                   0    Depletion of char supply.
                                   0    High char consumption  rates due to  mechanical  attrition.
                                   0    Correct/modify the char/sand screen separator.
                                   At this point the decision  was  made to prematurely terminate the FW-BF demonstration
                                   program rather than shut down,  debug, and restart  the  system again.  The  system
                                   supplier is pursuing additional funding  for the continuation of the prototype
                                   demonstration program.
                                            A-16
                                                                                  PEDCo EKYIRONMEHTW.

-------
          APPENDIX A
TERMINATED OPERATIONAL  FGD SYSTEMS
  IDENTIFICATION NO.
  UTILITY NAME
  UNIT NAME
  UNIT LOCATION
  UNIT RATING
ILLINOIS POWER
WOOD RIVER NO 4
EAST ALTON ILLINOIS
 110 MW
  FUEL CHARACTERISTICS  COAL   2.9-  3.2  PERCENT SULFUR
  FGO VENDOR
  PROCESS
  NEW OR RETROFIT
  START UP DATE
  F60 STATUS
  EFFICIENCY!
   PARTICULATES
MONSANTO ENVIRO  CHEM  SYSTEMS
CATALYTIC OXIDATION
RETROFIT
10/72
TERMINATED
 99 PERCENT
   S02
AS PERCENT
  WATER MAKE UP
  SLUDGE DISPOSAL
  UNIT COST
  OPERATIONAL
   EXPERIENCE
 SULFURIC ACID PRODUCT
 $82.5/KH CAPITAL + $952,000 OPERATING
THE FGD SYSTEM HAS HAD  CONSIDERABLE AMOUNT OF PROBLEMS SINCE STARTUP  IN
1972.  TOTAL OPERATION  WAS  
-------
                                                           BACKGROUND INFORMATION

                                                                     ON

                                                              WOOD RIVER NO.  4


     THE WOOD RIVER POWER STATION OF THE ILLINOIS POWER COMPANY IS LOCATED NEAR EAST  ALTON,  ILLINOIS,  NORTH OF  ST. LOUIS, MISSOURI.  THE NO. 4 BOILER

IS A COMBUSTION ENGINEERING PULVERIZED-COAL-FIRED UNIT THAT HAS A GROSS RATED CAPACITY  OF 109 MW AND A NET CAPACITY OF 103 MW.  THIS UNIT FIRES A HIGH

SULFUR CENTRAL ILLINOIS COAL WITH TYPICAL CHARACTERISTICS OF 3.1 PERCENT SULFUR, 10 PERCENT  ASH AND A  HEAT CONTENT OF 10,800 BTU/LB.  ANNUAL COAL

CONSUMPTION IS APPROXIMATELY 275,000 TONS/YEAR.

     THE EMISSION CONTROL EQUIPMENT FOR THIS BOILER INCLUDES MECHANICAL COLLECTORS, A HIGH EFFICIENCY  ESP, AND  A MONSANTO CATALYTIC OXIDATION  (CATOX)

FGD SYSTEM FOR THE CONTROL OF PARTICULATES AND SULFUR DIOXIDE.  DESIGN REMOVAL EFFICIENCIES  OF THIS CONTROL SYSTEM ARE 99.9 PERCENT FOR PARTICULATES AND

85 PERCENT FOR SULFUR DIOXIDE.  INLET SULFUR DIOXIDE CONCENTRATIONS TO THE CATOX SYSTEM ARE  GENERALLY  IN  THE  2000 TO 2200 PPM RANGE.

     FOLLOWING PASSAGE THROUGH THE PARTICULATE REMOVAL SYSTEM, THE FLUE GAS ENTERING  THE SCRUBBING SYSTEM IS  HEATED TO A TEMPERATURE OF 850°F AND

PASSES THROUGH A VANADIUM PENTOXIDE FIXED-BED CATALYTIC CONVERTER, WHERE THE SULFUR DIOXIDE  IS OXIDIZED TO SULFUR TRIOXIDE.  THE GAS THEN FLOWS THROUGH

AN ACID ABSORPTION TOWER, WHERE THE SULFUR TRIOXIDE IN THE GAS IS CONVERTED TO SULFURIC ACID.  AN ACID MIST ELIMINATOR ENSURES REMOVAL OF ENTRAINED

ACID MIST FROM THE GAS STREAM.  THE CLEANED GAS IS DISCHARGED TO THE STACK AND THE PRODUCT ACID IS COOLED AND STORED IN TANKS.  A SIMPLIFIED PROCESS

FLOW DIAGRAM OF THE WOOD RIVER CATOX SYSTEM IS PRESENTED IN FIGURE 25 OF APPENDIX  C.

     THIS DEMONSTRATION SYSTEM, PARTIALLY FINANCED BY EPA, WAS STARTED UP IN SEPTEMBER  1972. WHILE THE MAIN  PARTS OF THE UNIT HAVE PERFORMED ACCEPTABLY,

VARIOUS TROUBLES WITH ASSOCIATED EQUIPMENT HAVE CAUSED EXTENSIVE SHUTDOWNS AND DELAYS,  TO THE EXTENT THAT APPROXIMATELY 27 DAYS OF FULL OPERATION HAS

BEEN OBTAINED IN ALMOST TWO YEARS.  A 24-HOUR PERFORMANCE TEST RUN WAS COMPLETED IN JULY 1973.  THE FOLLOWING GUARANTEES WERE ACHIEVED AND  EXCEEDED:

90 PERCENT CONVERSION OF SULFUR DIOXIDE TO SULFUR TRIOXIDE (ABOUT 85 PERCENT NET REMOVAL); 99 PERCENT  REMOVAL OF PARTICULATE ENTERING THE SYSTEM; LESS

THAN 1 MG/ACF OF ACID MIST IN GAS LEAVING SYSTEM; PRODUCTION OF 60° BAUME1 ACID.

PERFORMANCE SUMMARY

     THE WOOD RIVER SYSTEM WAS STARTED UP IN SEPTEMBER 1972 BUT WAS SHUT DOWN ALMOST  IMMEDIATELY  (IN OCTOBER) TO CONVERT THE BURNERS TO OIL FIRING,

WHICH WAS NOT COMPLETED UNTIL JUNE 1973.  A SUCCESSFUL PERFORMANCE TEST WAS THEN MADE,  BUT BECAUSE OF  THE CATALYST PLUGGING HAZARD THE SYSTEM WAS' SHUT

DOWN AGAIN TO INSTALL AN EXTERNAL BURNER SYSTEM, WHICH WAS NOT COMPLETED UNTIL APRIL  1974.  VARIOUS OTHER PROBLEMS WITH STANDARD EQUIPMENT  HAVE BEEN

ENCOUNTERED SINCE, WITH THE RESULT THAT ONLY 657 HOURS OF OPERATING TIME HAVE BEEN LOGGED IN ALMOST TWO YEARS.



                                                                           A-18
                                                                                                                     PEDCo ENVIRONMENTAL

-------
MOOD RIVER NO. 4 (Continued)
     SEVERAL OTHER MAJOR PROBLEM AREAS ENCOUNTERED DURING THE INTERMITTENT OPERATION OF THIS REGENERABLE SYSTEM INCLUDED:   FROZEN  DAMPERS  ON  REHEAT
BURNERS, CRACKS IN THE TEFLON LINER ON THE ACID PUMP'S DISCHARGE HEADER, CRACKS IN THE REHEAT DUCTING, FALL OF REFRACTORY  BRICKS FROM THE  REHEATER
BURNER DOME, AND NEED FOR REINFORCEMENT OF THE STRUCTURE SUPPORTING THE HIGH TEMPERATURE FLUE GAS DUCT TO THE CATALYTIC CONVERTER.  MOST OF THESE
PROBLEMS HAVE BEEN CORRECTED.  ILLINOIS POWER AND EPA ARE NOW DETERMINING HOW TO CORRECT LEAKING ACID COOLERS.  PATCHING ATTEMPTS  HAVE  BEEN UNSUCCESSFUL.
REPAIR OR REPLACKENT OF THE COOLERS IS EXPECTED TO TAKE SEVERAL MONTHS.  EVALUATION FOR THE CONTINUATION OF FUTURE OPERATION IS STILL UNDER CONSIDERA-
TION.  A DECISION ON FUTURE OPERATIONS OF THIS SYSTEM WILL BE ANNOUNCED SHORTLY.
                                                                                                                         PEDCo ENVIRONMENTAL
                                                                          A-19

-------
                                           OPERATING LOG
                                    CATALYTIC OXIDATION SYSTEM
                               WOOD RIVER NO. 4 - ILLINOIS POWER CO..
                                           1972 TO 1973
                             System operating
System operating
Date
9-4-72
9-5-72
9-6-72
9-7-72
9-10-72
9-11-72
9-12-72
9-13-72
9-14-72
9-15-72
9-16-72
9-17-72
9-18-72
9-19-72
9-24-72
10-6-72
10-7-72
hours
12
24
24
2
6
2
16
24
24
24
24
24
24
3
17
12
24
Date
10-8-72
10-9-72
10-10-72
10-12-72
10-13-^72
10-14-72
10-30-72
10-31-72
7-21-73
7-22-73
7-23-73
7-24-73
7-25-73
7-26-73
7-17-73
7-28-73
7-29-73
hours
24
24
18
16
20
16
24
16
18
24
18
24
14
13
19
19
9
NOTE:  The operation time log does  not  Include Intermittent system operation during
       1974.  System operations for 1974 amounted to 55 hours.  Total operation
       time for 2.5 years of operation  was 657 hours.
                                                 A-20
                                                                                           PEDCo ENVIRONMENTAL

-------
               APPENDIX A
  TERMINATED OPERATIONAL  F6D  SYSTEMS
IDENTIFICATION NO.

UTILITY NAME

UNIT NAME
UNIT LOCATION

UNIT RATING
 POTOMAC ELECTRIC * POWER

 DICKERSON NO 3

 DlcKERSON MARYLAND

   95 MW
FUEL CHARACTERISTICS   COAL    2.0 PERCENT SULFUR
F6D VENDOR

PROCESS

NEW OR RETROFIT

START UP DATE

FGD STATUS

EFFICIENCY.
 PARTICULATES
 CHEMICO

 MAGNESIUM OXIDE  SCRUBBING

 RETROFIT

  9/73

 TERMINATED

 99.3 PERCENT
 S02
 90 PERCENT
WATER MAKE UP
SLUDGE DISPOSAL
                       3.2 GPM/MW
 ACID PLANT REGENERATION
UNIT COST
S70/KW CAPITAL
OPERATIONAL
 EXPERIENCE
 REFER TO BACKGROUND INFORMATION SECTION  IN APPENDIX A OF THIS REPORT.  THIS
 FGO SYSTEM HAS BEEN OPERATIONAL SINCE  SEPTEMBER 1973. THE UNIT HAS BEEN
 TERMINATED AS AN S02 SCRUBBER. HOWEVER.IT  WILL CONTINUE TO OPERATE AS A
 PARTICULATE SCRUBBER.
                                                                                                      PEDCo ENVIRONMENTAL
                                                              A-21

-------
                                                                BACKGROUND  INFORMATION

                                                                         ON

                                                                    DICKERSON NO.  3


     THE DICKERSON STATION OF POTOMAC ELECTRIC POWER CO.  (PEPCO) IS LOCATED ON THE POTOMAC RIVER NEAR DICKERSON, MARYLAND, ABOUT 30 MILES NORTHWEST OF

WASHINGTON, D.C.  THE STATION HAS THREE ELECTRIC GENERATORS,  EACH RATED  AT  190 MU.  UNIT NO.  3  IS A DRY BOTTOM COAL-FIRED BOILER DESIGNED BY COMBUSTION

ENGINEERING AND INSTALLED IN 1962.  THE COAL NOW BURNED HAS AN AVERAGE GROSS HEATING VALUE OF 11,700 BTU/LB AND AVERAGE ASH AND SULFUR CONTENTS OF

14 AND 2 PERCENT, RESPECTIVELY.  THE BOILER IS FITTED WITH AN ELECTROSTATIC PRECIPITATOR DESIGNED AND INSTALLED BY RESEARCH-COTTRELL IN 1962.  THE FGD

SYSTEM EMPLOYS THE CHEMICO-BASIC MAGNESIUM OXIDE SCRUBBING PROCESS.  THE RETROFIT  SYSTEM HANDLES APPROXIMATELY 50 PERCENT OF THE EXHAUST GAS FROM THE

NO. 3 UNIT.

     THE FGD SYSTEM CONSISTS OF A SINGLE, TWO-STAGE SCRUBBER/ABSORBER, WHICH INCORPORATES AN  ADJUSTABLE-THROAT VENTURI SCRUBBER FOR PARTICULATE

REMOVAL AND A SECOND STAGE ABSORBER WITH A FIXED VENTURI  TO REMOVE 3ULFUR DIOXIDE. THE LIQUOR  STREAMS FOR BOTH STAGES ARE SEPARATE AND OPERATE IN A

CLOSED-LOOP MODE.  UNTIL MID-1975 THE MAGNESIUM SULFITE GENERATED WAS TRANSFERRED  TO AN EPA FINANCED FACILITY AT THE ESSEX CHEMICAL COMPANY SULFURIC

ACID MANUFACTURING PLANT IN RUMFORD, RHODE ISLAND,  WHERE  MAGNESIUM OXIDE WAS REGENERATED AND  SUFLUR DIOXIDE FROM THE REGENERATION PROCESS WAS CONVERTED

TO SULFURIC ACID.  THE RUMFORD FACILITY HAS SINCE BEEN CLOSED DOWN.  A GENERAL PROCESS FLOW DIAGRAM OF THE DICKERSON NO. 3 WET SCRUBBING SYSTEM AND

REGENERATION FACILITIES IS PRESENTED IN FIGURE 25 OF APPENDIX C.

     CONSTRUCTION WAS COMPLETED IN AUGUST AND THE SYSTEM  STARTED UP IN SEPTEMBER 1973.  DURING  INTERMITTENT OPERATIONS FOR SHAKEDOWN THROUGH JANUARY

1974, THE SYSTEM'S LONGEST CONTINUOUS RUN WAS 271 HOURS.   THE SYSTEM WAS RESTARTED FROM JULY  THROUGH DECEMBER 1974, AND AGAIN ON AUGUST 11, 1975, FOR

APPROXIMATELY 87 HOURS.

     FGD UNIT OUTAGES WERE CAUSED PRIMARILY BY PIPE AND PUMP  CORROSION AND  MAJOR TURBINE OVERHAUL OF THE  BOILER.  PARTICULATE AND SULFUR DIOXIDE REMOVAL

EFFICIENCY GUARANTEES WERE CORROBORATED DURING OPERATIONAL PHASES.

     THE REMAINING SUPPLY OF MAGNESIUM OXIDE, ABOUT 100 TONS  (10 DAYS),  HAS BEEN DEPLETED. AND  THE DICKERSON UNIT HAS BEEN TERMINATED AS AN FGD SYSTEM.
                                                                            A-22
                                                                                                                          PEDCo ENVIRONMENTAL

-------
                                                          DICKERSON NO. 3
                                                   FGD SYSTEM OPERATING HISTORY

Operating Period                                                      Comments
Sep. 73                  Problems during this period ranged from corrosion leaks in expansion joints to problems in material
  to                     handling equipment, feeding and slaking of MgO, plugging in the MgO mix tank and suction lines, to
Jan. 74                  the MgO make-up pumps.

Jan. 74                   Maintenance and modifications were performed on the system.  The major system revision made during
  to                      this period was the addition of a pre-mix tank in the MgO system.
Apr. 74

Apr. 74                   Limited operation  because  the utility did not have access to the EPA calcining facility at the Essex
  to                      Chemical  Company sulfuric  acid plant.  By the end.of June 1974, all the MgO at Dickerson had been used
Jul. 74                   and a silo plus three train cars were full of MgSOj.

Aug. 74                   During this period the system generally operated at 75 percent of the design gas flow.
  to
Dec. 74

Jan. 75                   Problems developed in the bucket elevator transporting the MgSO- from the dryer to the storage silo.

Feb.   75                  Unit No. 3 was taken out of service for an 8 to 12 week turbine overhaul.  The scrubber was inspected,
  to                      maintenance and modifications were made.
Jul. 75
                                                                 A-23
                                                                                                            PEDCo ENVIRONMENTAL

-------
                                               DICKERSON NO. 3 (Continued)
                                              F6D SYSTEM OPERATING HISTORY

Operating Period                                                      Comments
Aug. 75                   The FGD system was restarted 1n August.  Steam was lost to the MgO mix tank, resulting in a very moist
                          product from the centrifuge.   Caking in the dryer occurred.  At this point, the utility decided to test
                          only the first-stage of the scrubbing system, taking gas ahead of the precipitator.  FGD operation at
                          Dickerson terminated at this point.
                                                                                                          PEDCo ENVIRONMENTAL

-------
       APPENDIX A
  TERMINATED OPERATIONAL F60 SYSTEMS
IDENTIFICATION NO.
UTILITY NAME
UNIT NAME
UNIT LOCATION
UNIT RATING
FUEL CHARACTERISTICS
F60 VENDOR
PROCESS
NEW OR RETROFIT
START UP  DATE
FGD STATUS
EFFICIENCYt
 PARTICIPATES

 S02
WATER  HAKE  UP
SLUDGE  DISPOSAL
UNIT COST
 OPERATIONAL
  EXPERIENCE
SOUTHERN CALIFORNIA EDISON
MGHAVE NO 1A
LAboHLIN NEVADA
 170 nw
COAL   0.5- 0.8 PERCENT  SULFUR
UNIVERSAL OIL PRODUCTS
LIMESTONE SCRUBBING
RETROFIT
11/7H
 TERMINATED
93 PERCENT

95 PERCENT

0.92 GPM/MW

EXPERIMENTAL METHODS

NOT AVAILABLE
THIS  EXPERIMENTAL  MODULE  STARTED UP OCT.  31,  197<* AND OPERATED WITH AN
AVAILABILITY  OF  60.t*  THROUGH FOUR  MONTHS OF  TESTING.  TESTS HAVE BEEN
COMPLETED,  AND THE FGD SYSTEM WAS SHUT  DOWN INDEFINITELY ON JULY 2, 197S.
NEVADA  ASSEMBLY  BILL NO.  708 HAS PLACED A 2-YEAR MORATORIUM ON THE
ENFORCEMENT OF THE COMPLIANCE SCHEDULE  FOR THIS STATION.  FURTHER FGD
ACTIVITIES  WILL  BE DEPENDENT ON FUTURE  LEGISLATION*
                                                                                                 PEDCo ENVIRONMENTAL
                                                              A-25

-------
             APPENDIX A
TERMINATED OPERATIONAL FGD SYSTEMS
IDENTIFICATION NO.       8
UTILITY NAME
UNIT NAME
UNIT LOCATION
UNIT RATING
FUEL CHARACTERISTICS
FGD VENDOR
PROCESS
NEW OR RETROFIT
START UP DATE
FGD STATUS
EFFICIENCY,
 PARTICULATES
 so2
WATER MAKE UP
SLUDGE DISPOSAL
UNIT COST
OPERATIONAL
 EXPERIENCE
SOUTHERN CALIFORNIA EDISON
MOHAVE NO. 2A
LAUGHLIN NEVADA
160 MW
COAL   0.5- 0.8 PERCENT SULFUR
SCE/ STEARNS ROGER
LIME SCRUBBING
RETROFIT
11/73
TERMINATED
93 PERCENT

95 PERCENT
1.0 GPM/MW
STABILIZED SLUDGE DISPOSED  IN UNLINED  POND
NOT AVAILABLE

SINCE STARTUP OF FORMAL TEST PROGRAM ON  JANUARY  16. 1974, AND  UP  TO  DECEMBER 20, 1974,THIS EXPERIMENTAL
HORIZONTAL MODULE OPERATED  5280 HRS. WITH AN  OVERALL  AVAILABILITY  OF  77.4 PERCENT,  SOz REMOVAL
EFFICIENCY WAS 90 IN FLUE GAS TO SIMULATE CONDITIONS  FROM COMBUSTION  OF  HIGH SULFUR COAL.   THIS FGD
SYSTEM OPERATED FROM NOVEMBER 1973 UNTIL FEBRUARY  1975.   FGD PLANS AT THIS STATION  WILL BE BASED
ON INFORMATION THAT INCLUDES OPERATIONAL DATA THAT HAVE  BEEN OBTAINED DURING THE FGD TEST  PROGRAMS
AT THE MOHAVE STATION.  THE PHOTOTYPE  SYSTEM  AT  MOHAVE  IS NOW BEING DISMANTLED AND  IS BEING SHIPPED
TO THE FOUR CORNERS PLANT,  OPERATED BY ARIZONA PUBLIC SERVICE,  FOR INSTALLATION.
                                                                                                          PEDCo ENVIRONMENTAL
                                                               A-26

-------
                                                           BACKGROUND INFORMATION
                                                                     ON
                                              THE MOHAVE TEST MODULES PROGRAM:   NOS.  1A AND  2A

     TWO PROTOTYPE SULFUR DIOXIDE ABSORBER MODULES WERE INSTALLED IN 1973 AT THE MOHAVE GENERATING STATION  OF THE SOUTHERN CALIFORNIA EDISON
COMPANY.  A VERTICAL MODULE, RATED AT 170 MW, WAS INSTALLED TO TREAT 450,000 SCFM PORTION OF THE FLUE  GAS FROM UNIT NO. 1.  A HORIZONTAL MODULE,
ALSO RATED AT 170 MW, WAS INSTALLED TO TREAT A SIMILAR FLUE GAS PORTION FROM UNIT NO. 2.  UNITS 1  AND  2  ARE IDENTICAL  BOILERS, EACH HAVING A
MAXIMUM NET CONTINUOUS GENERATING CAPACITY OF 790 MW AND EACH BURNING A WESTERN, LOW-SULFUR  COAL WITH  A  HEATING VALUE  OF 11,500 BTU/LB AND ASH
AND SULFUR CONTENTS OF 10 AND  0.4 PERCENT RESPECTIVELY.
VERTICAL MODULE
     THE VERTICAL MODULE, A UNIVERSAL OIL PRODUCTS TURBULENT CONTACT ABSORBER (TCA),  WAS TESTED IN TWO MODES:  FIRST,  AS A TCA UNIT, FROM NOVEMBER
2, 1974 TO APRIL 30, 1975, AND SECOND AS A POLYGRID PACKED ABSORBER (PPA), WHEN THEN  THE "PING PONG BALLS"  WERE REPLACED WITH A PLASTIC "EGGCRATE"
PACKING WITH TESTING CONTINUING TO JULY 2, 1975.
     STARTUP OF THE VERTICAL MODULE WAS INITIATED ON SCHEDULE JANUARY 1, 1974.   ON JANUARY 24, 1974, A FIRE BURNED MOST OF THE CHLOROBUTYL
LINING AND SYSTEM RESTART WAS DELAYED UNTIL OCTOBER 1, 1974.  TESTING OF THIS MODULE  FOLLOWED A MONTH  LATER AND WAS COMPLETED AFTER 3,131 HOURS
OF OPERATION.  THE MODULE IS PRESENTLY SHUT DOWN IN A COLD STAND-BY CONDITION AT THE  MOHAVE  GENERATING STATION.
HORIZONTAL MODULE
     THE HORIZONTAL MODULE, A FOUR-STAGE HORIZONTAL CROSSFLOW SPRAY SCRUBBER, WAS OPERATED BY THE  UTILITY IN A SHORT SERIES OF STARTUP TESTS THAT
ENDED ON JANUARY 16, 1974, WHEN A FORMAL TEST PROGRAM WAS INITIATED TO ASSESS THE PERFORMANCE AND  RELIABILITY CHARACTERISTICS OF THE SCRUBBING
SYSTEM.  THE TEST PROGRAM WAS TERMINATED ON FEBRUARY 9, 1975, FOLLOWING 5,927 HOURS OF OPERATION.   THE MODULE WAS SUBSEQUENTLY DISMANTLED,
TRANSPORTED, AND REASSEMBLED AT THE FOUR CORNERS PLANT OF ARIZONA PUBLIC SERVICE WHERE ADDITIONAL  TESTING IS NOW BEING CONDUCTED.
     INFORMATION AND DATA CONCERNING THE PERFORMANCE OF THE MOHAVE TEST MODULES ARE GIVEN IN THE FOLLOWING  PERFORMANCE TABLES.  PROCESS FLOW DIAGRAMS
OF THE TEST MODULES ARE PROVIDED IN FIGURES  27 AND 28 OF APPENDIX C.
                                                                                                                     PEDCo ENVIRONMENTAL
                                                                            A-27

-------
                          MOHAVE NO. 1A - VERTICAL TEST MODULE

                  OUTAGE TIME  HISTORY:  NOVEMBER 2, 1974 TO JULY 2, 1975
                    Reason                                   Time (hr)
1.   Repair grids and redistribute TCA balls                    710
2.   Clean scale from scrubber internals                        344
3.   Repair/replace plugged  nozzles                             153
4.   Repair leaks in trap-out  tray                              120
5.   Repair/realign PPA packing                                 85
6.   Correct booster fan trip  problems                           72
7.   Conduct inspections for extended operations                 46
8.   Remove hardhat from thickener                               46
9.   Total outage time                                        1585

     Total outage time:  1585  hours
     Total calendar time:   5813 hours
     Total operational time:  4228  hours
     Percent availability:   72.73
                                                 A-28
                                                                                      PEDCo ENVIRONMENTAL

-------
                          MOHAVE  NO. 2A - HORIZONTAL TEST MODULE

                 OUTAGE  TIME  HISTORY:  JANUARY 16, 1974 TO FEBRUARY 9, 1975
                     Reason                                       Time (hr)
 1.    Modify and repair  plastic  demister blades                      503
 2.    Correct booster fan balance  problems                           317
 3.    Pump repair                                                   256
 4.    Spray nozzle replacement                                      238
 5.    Modify gas Inlet flow distribution                             162
 6.    Repair hopper leaks                                           135
 7.    Remove hardhat from thickener                                  82
 8.    Modify slaking water for scale prevention                       45
 9.    Conduct inspections for extended operations                   	19_
10.    Total outage time                                             1757

      Total outage time:  1757 hours
      Total calendar time:  9328 hours
      Total operating time:   7571  hours
      Percent availability:   81.162
                                            A-29
                                                                               PEDCo ENVIRONMENTAL

-------
            APPENDIX A

  TERMINATED OPERATIONAL  FGD SYSTEMS

IDENTIFICATION NO.     9

                       TENNESSEE VALLEY AUTHORITY
                                  -^

                       SHAWNEE  NO.  IOC

                       PADUCAH  KENTUCKY

                         10 MW
UTILITY NAME

UNIT NAME
UNIT LOCATION

UNIT RATING
FUEL CHARACTERISTICS   COAL  2.9 PERCENT SULFUR
FGD VENDOR

PROCESS

NEW OR RETROFIT

START UP DATE

FGD STATUS

EFFICIENCY,
 PARTICULATES


 S02


WATER MAKE UP


SLUDGE DISPOSAL
                      TENNESSEE VALLEY AUTHORITY

                      LIME/LIMESTONE SCRUBBING

                      RETROFIT

                       H/72

                      OPERATIONAL

                      EXPERIMENTALLY CONTROLLED



                      EXPERIMENTALLY CONTROLLED


                      EXPERIMENTALLY CONTROLLED


                      EXPERIMENTALLY CONTROLLED
UNIT COST
OPERATIONAL
 EXPERIENCE
                      REFEK  TO  BACKGKOUND INFORMATION  SECTION  IN APPENDIX C.  THIS
                      FGO  SYSTEM HAS liEEN OPERATIONAL  SINCE  APRIL.1972.  THIS MARBLE-BED AB-
                      SORBER, MANUFACTURED BY COMBUSTION  ENGINEERING CO.,  WAS DISCONTINUED
                      EARLY  IN  THE TEST PROGRAM BECAUSE OF CONTINUED OPERATING PROBLEMS WITH
                      NOZZLE FAILURE AND SUBSEQUENT PLUGGING OF THE MARBLE BED.  THIS SYSTEM
                      BECAME OPERATIONAL IN APRIL 1972 AND WAS PERMANENTLY TERMINATED IN
                      JULY 1973.
                                                                                                           PEDCo ENVIRONMENTAL
                                                                 A-30

-------
                                                           BACKGROUND INFORMATION

                                                                     ON

                                                       SHAWNEE NOS. IDA, 10B,  AND IOC



     IN JUNE 1968, THE EPA INITIATED A PROGRAM TO TEST PROTOTYPE WET LIME AND  LIMESTONE SCRUBBING SYSTEMS FOR REMOVAL OF  SULFUR DIOXIDE AND PARTICULATES

FROM FLUE GAS.  THE PROGRAM WAS CARRIED OUT IN A TEST FACILITY INCORPORATED INTO THE FLUE GAS DUCT WORK OF UNIT NO.  10, A COAL-IFRED BOILER AT THE

TVA SHAWNEE POWER STATION, PADUCAH, KENTUCKY.  TVA IS THE CONSTUCTOR AND FACILITY OPERATOR AND THE BECHTEL CORP. IS  THE MAJOR  CONTRACTOR AND TEST

DIRECTOR.

     THE TEST FACILITY CONSISTS OF THREE PARALLEL SCRUBBER SYSTEMS OF PROTOTYPE SIZE TREATING PART OF THE FLUE GAS FROM THE  BOILER.  EACH SCRUBBER

TRAIN IS CAPABLE OF TREATING APPROXIMATELY 30,000 ACFM, OR THE EQUIVALENT OF APPROXIMATELY 10 MW OF POWER PLANT GENERATING CAPACITY.

     THREE PARALLEL WET SCRUBBER SYSTEMS WERE SELECTED FOR THE TEST PROJECT:  1) A VENTURI WITH A SPRAY TOWER AFTER  ABSORBER;  2) A TURBULENT CONTACT

ABSORBER (TCA) AND 3) A MARBLE-BED ABSORBER.  THE VENTURI SYSTEM, MANUFACTURED BY CHEMICAL CONSTRUCTION CO.,  CONTAINS AN  ADJUSTABLE THROAT THAT PERMITS

CONTROL AND VARIATION OF PRESSURE DROP UNDER A WIDE RANGE OF FLOW CONDITIONS.   THE TCA UNIT,  MANUFACTURED BY  UNIVERSAL OIL PRODUCTS, EMPLOYS A

FLUIDIZED BED OF LOW DENSITY PLASTIC SPHERES THAT ARE FREE TO MOVE BETWEEN RETURNING GRIDS.  THE MARBLE-BED ABSORBER, SUPPLIED BY COMBUSTION ENGINEERING

CO., USES A PACKING OF 3/4-INCH GLASS MARBLE SPHERES AND A TURBULENT LAYER OF  LIQUID AND GAS  ABOVE THE MARBLE LAYER  TO ENHANCE MASS TRANSFER.

     THE TEST FACILITY WAS DESIGNED SO THAT MODIFICATIONS AND VARIATIONS OF SCRUBBER INTERNALS AND PIPING COULD BE READILY EMPLOYED FOR EACH SCRUBBER

SYSTEM.  EACH SYSTEM CAN TREAT APPROXIMATELY 30,000 ACFM OF FLUE GAS AT 300°F  CONTAINING 1800 TO 4000 PPM OF  S02 AND 2 TO 5  GRAINS/SCF OF PARTICULATES.

TESTING OF THE TCA AND THE VENTURI SPRAY TOWER IS IN PROGRESS; OPERATION OF THE MARBLE-BED ABSORBER UNIT HAS  BEEN PERMANENTLY  DISCONTINUED.
                                                                                                                       PEDCo  ENVIRONMENTAL
                                                                            A-31

-------
A-32

-------
 APPENDIX b

FGU ECONOMICS
    B-l
                           PEDCO-ENVIRONMENTAL

-------
B-2

-------
                                                        APPENDIX B.   FGD SYSTEMS ECONOMICS
COMPANY
PLANT
UNITS
TOTAL CAPACITY, MW
Alabama Electric Coop.
Tombigbee Power Station
Nos. 2 & 3
450

Arizona Public Service
Choi la Electric Generating
Station
No. 1
115

Boston Edison Company
Mystic Power Station
No. 1
155





PROCESS
STATUS
START-UP DATE
Limestone
Construction
3/78 & 3/79

Limestone
Operational
10/73

Magnesium Oxide
Terminated
4/72





REPORTED CAPITAL
COSTS,
$ MILLION
40.464

6.555

9.510





$/KW
89.92

57.0

63.4





REPORTED OPERATING
COSTS,
$ ANNUAL
240,323



615,000





MILLS/KWH
0.77

2.20

3.0





COMMENTS
1. Capital cost figures include upstream particulate con-
trol equipment (ESP's).
2. 7Q% of the flue gas capacity is scrubbed.
3. Annual operating costs are calculated for 1978 with a
60% boiler capacity factor.
1. Capital cost figure includes the venturi scrubbers (2)
for particulate control. This figure represents
total expenditures made by the utility through 1973.
2. Capital cost figure does not include limestone prep-
aration and sludge handling facilities and interest
on capital during construction.
3. Additional costs incurred by the system supplier have
not been reported.
1. All cost figures are reported for the project com-
pletion date of 1974.
2. The total installed capital cost of the Rumford cal-
cination facility was approximately $4.5 MM.
3. Capital charges are not included because of non-
applicability to a 2-year demonstration program.
4. Operating costs for the acid plant regeneration
facility are not included.
5. The cost of make-up magnesium oxide ($150/T) are not
included.
6. 3.0 mills/kWh is an estimate for total operation and
maintenance costs, including calcination.
7. BECO and EPA each subsidized approximately 50% of the
costs of the demonstration program. Chemico also
underwrote some of the program costs.
Note:  N/A indicates  figures are not available.
                                                                          B-3
                                                                                                                     PEDC6 ENVIRONMENTAL

-------
                                                    APPENDIX B (Continued).   FGD SYSTEMS ECONOMICS
COMPANY
PLANT
UNITS
TOTAL CAPACITY, MW
Big Rivers Electric Coop
Reid Steam Station
No. 2
280






Central Illinois Light Co.
Duck Creek Power Plant
No. 1
400




Central Illinois Public Serv.
Newton Station
No. 1
575







PROCESS
STATUS
START-UP DATE
Lime
Contract
Awarded
1979






Limestone
Operational,
Construction
9/76 & 8/78




Double Alkali










REPORTED CAPITAL
COSTS,

$ MILLION
16









36







48.875











$/KW
64









90







85










REPORTED OPERATING
COSTS,

$ ANNUAL










N/A







13.425 MM











MILLS/KWH


















3.81












COMMENTS
1. The reported capital cost figure applies to the amount
of the contract awarded to AAF for a turnkey emission
control installation.

2. The figure includes an AAF-ELEX ESP, two spray towers,
reheater, ancillary equipment, ductwork, and molecular
pre-wired control rooms.
3. All figures are reported in 1976 dollars.
4. Escalation factors, costs, and indirect costs are not
included.
1. The capital cost figure is an estimate of expend-
itures, including $4.0 MM for the ESP, and the cost of
the limestone milling and waste disposal facilities.

2. One module has been completely installed and tempo-
rarily started-up in September 1976. The remaining
three modules are scheduled for operation in August
1978.
1. The capital cost figure is an estimate for total
projected expenditures. Since construction has re-
cently commenced, exact figures are not available.
Total expenditures may well run higher than the $85/kW
posted in the table.
2. Cost to own and operate figures are projections based
upon firing the design coal (10,900 Btu/lb, 4% S,
0.2% Cl at a load factor of 7055 with a system SO?
removal efficiency of 95%. Full load heat release is
5500 MM Btu/hr. Stack exit temperature is 154°F.
System lifetime is 30 years.
Note:  N/A indicates figures are not available.
                                                                                                                    PEDCo ENVIRONMENTAL
                                                                           B-4

-------
                                                   APPENDIX  B  (Continued).   FGD SYSTEMS  ECONOMICS
COMPANY
PLANT
UNITS
TOTAL CAPACITY, MW
Columbus & So. Ohio Electric
Conesville Generating Station
Nos. 5 & 6
800


Colorado Ute Electric
Craig Station
Nos. 1 & 2
900


Commonwealth Edison
Powerton Station
No. 51
425


PROCESS
STATUS
START-UP DATE
Lime
Construction
12/76 & 1/78


Not selected
Considering
Spring, 1979


Limestone
Contract
Awarded


REPORTED CAPITAL
COSTS,
$ MILLION
38.661


105


50


$/KW
48.32


117


117.65


REPORTED OPERATING
COSTS,
$ ANNUAL
7.826 MM


15 MM





MILLS/KWH
2.83





8.70


COMMENTS
1. The capital cost figure includes direct costs only.
2. The electrostatic precipitators are also included
in the capital cost figure ($4.973 MM for 2 units).
3. Annual operating costs are estimated for both units at
a load factor of 39.5%.
4. The cost estimates are given in 1975 dollars.
1. The total capital cost figure is an estimate provided
by the utility that does not include limestone
preparation and sludge disposal facilities. This
figure is based upon a non-regenerable SO. scrubbing
system (lime/limestone).
2. Electrostatic precipitators are included in the
capital cost figure.
3. The annual operating cost figure is a utility es-
timate also based upon the installation of a non-
regenerable SO- scrubbing system.
1. The total installed capital cost expenditures apply
to the following timetable: all expenditures will be
made from May 1976 to December 1978; expenditures
of $16 MM will be made from October 1976 to October
1977.
2. The annual operating cost is an estimate which in-
cludes the following items:
2.7 mills/kWh for operation and maintenance.
6.0 mills/kWh for auxiliary power requirements.
Scrubber life span is estimated for an annual
usage rate of 148,000,000 kWh.
Note:  N/A Indicates figures are not available.
                                                                                                                   PEDCo ENVIRONMENTAL
                                                                         B-5

-------
                                                  APPENDIX  B  (Continued).  FGO SYSTEMS ECONOMICS
COMPANY
PLANT
UNITS
TOTAL CAPACITY, MW
Commonwealth Edison
Will County Station
No. 1
167







Detroit Edison
St. Clair Plant
No. 6
163 MW




Duquesne Light
F.R. Phillips Station
Nos. 1 to 6
410 MW

Elrama Station
Nos. 1 to 4
510 MW













PROCESS
STATUS
START-UP DATE
Limestone
Operational
2/72








Limestone
Operational
5/76





Lime
Operational
7/73


Lime
Operational
10/75













REPORTED CAPITAL
COSTS,

$ MILLION
15.542










14.996







40




42
















$/KW
113










92







103




93















REPORTED OPERATING
COSTS,

$ ANNUAL
3.985 KM










2.139 KM










32 MM


















MILLS/KWH
13.06










2.3










6.0



















COMMENTS
1. The capital cost figure includes the venturi scrubbers
for particulate control.

2. The annual operating cost figure is based on a
system lifetime of 14 years. Sludge treatment costs
include hauling to an off-site disposal area. The
figure provided is the cost to own and operate the
scrubbing system for 1975.
3. The $/kW figure is based upon the unit's maximum net
generating capacity with the FGD system, 137 MW.
4. Unit load capacity factor for 1975 was 49.4%.
1. The total capital cost figure includes expenditures
made through 1976.

2. Because of demonstration status, limestone preparation
facilities are not required and a disposal pond
capacity of 1 year is necessary.
3. Operating costs are estimates for operation during
1975 at a unit load factor of 65%.
1. Total capital cost figure for Phillips includes
expenditures of $32 million through 1975 and an addi-
tional $8 million required to bring the entire
plant into compliance. The figure for Elrama includes
expenditures of $34 million through 1975 and an
additional $12 million required to bring the entire
plant into compliance.

2. Total capital cost figures include all process equip-
ment, engineering costs, contractor's fees and interest
on capital during construction. Excluded are the
costs of additional sludge disposal facilities that
may be required. The $/kW values are based upon the
station's net generating capacities with the scrubbers
in service. The Phillips station net generating
capacity is 387 MW. Elrama's net generating capacity
is 494 MW.
3. Annual operating cost figures of 6 mills/kWh is based
upon the combined operating costs for the Phillips and
E1ra.ua stations when full S02 compliance is achieved.
This amounts to approximately $32 million.
Note:  N/A indicates  figures are not available.
                                                                          B-6
                                                                                                                      PEDCo ENVIRONMENTAL

-------
                                                   APPENDIX  B (Continued).   FGD  SYSTEMS  ECONOMICS
COMPANY
PLANT
UNITS
TOTAL CAPACITY, MM
General Motors
Chevrolet Parma Plant
Nos. 1,2,3 & 4




Gulf Power
Scholz Steam Plant
Nos. 1 & 2
23

Gulf Power
Scholz Steam Plant
No. 2
20

Illinois Power
Wood River Power Station
No. 4
110








PROCESS
STATUS
START-UP DATE
Double Alkali
Operational
3/74




Dilute Acid,
Operational
2/75


Dry Adsorption
Terminated
2/76


Catalytic
Oxidation
Terminated
10/72








REPORTED CAPITAL
COSTS,

J MILLION
3.2






3.0




N/A




8.5












$/KW
100






130




N/A




82.5











REPORTED OPERATING
COSTS,

$ ANNUAL
643,500






N/A




N/A




952,000












MILLS/KWH







N/A




N/A


















COMMENTS
1. Total capital cost figure includes all expenditures
made on the system through 1975.

2. Annual cost figure is based upon the consumption of
55,000 tons/year- of high sulfur (2.0 to 2.5%) eastern
Ohio coal in the boilers. This equals approximately
$11.70 per ton of coal consumed at the plant.
1. The total installed capital cost figure provided for
the CT-101 prototype unit includes the scrubbers and
ancillary equipment, engineering costs and contractors
fee. This figure is not representative of a full-
scale application.
1. Actual cost figures for this prototype unit are not
available. Foster Wheeler has published initial
capital cost figures which range from $25 to $35 per
kW for low sulfur removal efficiency and $70 to $75
per kW for high sulfur removal efficiency.
1. Reported capital cost figure represents the total
expenditures during the 2.5 year duration of the
program.

2. The $/kW figure is based upon the system's net
generating capacity of 103 MW.
3. ESP cost is included since upstream fly ash removal
is a necessary feature of this regenerable system.
4. The annual cost figure is an estimate representing
system running costs only. Excluded are capital
charges and a credit for product. This figure trans-
lates into a value of $3.46 per ton of coal consumed.
Note;  N/A Indicates figures are not available.
                                                                                                                   PEDCo ENVIRONMENTAL
                                                                         B-7

-------
                                                    APPENDIX B (Continued).   FGD  SYSTEMS  ECONOMICS
COMPANY
PLANT
UNITS
TOTAL CAPACITY, MW
Indianapolis Power & Light
Petersburg Generating Station
No. 3
530

Kansas City Power & Light
Hawthorn Power Station
Nos. 3 & 4
525

Kansas City Power & Light
La Cygne Power Station
No. 1
820

PROCESS
STATUS
START-UP DATE
Limestone
Construction
9/77

Limestone
Injection &
Wet Scrubbing
Operational
11/72

Limestone
Operational
2/73

REPORTED CAPITAL
COSTS,
$ MILLION
36.885

5.32

52.4

$/KW
69.9

19

63.9

REPORTED OPERATING
COSTS,
$ ANNUAL




1.79 MM

MILLS/KWH


2.2-2.5

0.94

COMMENTS
1. Capital cost figure includes the ESP's installed
upstream for primary particulate control.
2. Interest during construction is not included.
3. FGD design and costs are based upon 4.5% sulfur coal,
which is the maximum allowable for the system.
1. This figure is unrealistically low because these
installations are experimental in nature and were
heavily underwritten by the system supplier.
2. Sludge disposal facilities are not included in the
total cost figure.
3. The annual operating cost figure does not include
fixed costs.
1. The capital cost figure includes $45.4 million in
expenditures already made plus an additional $7
million required to reach optimum system performance
($5.2 million for the installation of an eighth
scrubber module).
2. The annual operating cost figures are estimates for
1976 operations based upon extrapolation of first
quarter figures provided by the utility. Included are
operating labor and materials, maintenance labor and
materials, and limestone.
Note:  N/A Indicates figures are not available.
                                                                                                                        PEDCo ENVIRONMENTAL
                                                                           B-8

-------
                                                    APPENDIX B (Continued).   FGO  SYSTEMS  ECONOMICS
COMPANY
PLANT
UNITS
TOTAL CAPACITY, HW
Kansas Power & Light
Lawrence Energy Center
Nos. 4 & 5
525 HW




Kentucky Utilities
Green River Power Station
Nos. 1 & 2
64

Key West Utility
Stock Island Power Plant
37











PROCESS
STATUS
START-UP DATE
Limestone
Injection &
Wet Scrubbing
Operational
12/68 & 11/71




Lime
Operational
9/75

Limestone
Operational
10/72











REPORTED CAPITAL
COSTS,
$ MILLION
3.5




3.996

0.750











$/KW
7




62.44

20.7











REPORTED OPERATING
COSTS,
$ ANNUAL
N/A


















MILLS/KWH
N/A




2.0

0.7













COMMENTS
1. The capital cost figure presented represents a sum
paid by the utility for both systems in 1968. Ex-
penses incurred in many subsequent modifications
over the years were largely underwritten by the
system supplier. Therefore, the figures listed are
unreal istically low and are not meaningful.
2. These units are now being replaced with venturi rod
scrubber and spray tower systems. The total installed
costs for these systems are not available.
1. The capital cost figure for this turnkey installa-
tion does not include the utility's expenditures
for engineering, operator training, and other indirect
cost factors.
1. This system was jointly funded by the EPA and the
utility. The system supplier has also underwritten
a considerable amount of the capital expenditures.
This figure, therefore, Is unreal Istically low.
2. The utility has had to pay for the cost of a new
primary crushing system.
3. The operating cost figure provided was an original
estimate and has not been corroborated or disputed
by actual experience. This estimate was based upon
the following factors:
Capitalization rate of 10%; no taxes, no insurance.
Maintenance cost of 5% of equipment cost.
Labor cost at $20,000 per year.
Limestone cost at $4.05 per ton.
Note:  N/A Indicates figures are not available.
                                                                                                                   PEDCo ENVIRONMENTAL
                                                                         B-9

-------
                                                  APPENDIX B  (Continued).  FGD SYSTEMS ECONOMICS
COMPANY
PLANT
UNITS
TOTAL CAPACITY, MW
Louisville Gas & Electric
Cene Run Power Station
No. 4
178
Louisville Gas & Electric
Cane Run Power Station
No. 5
183
Louisville Gas & Electric
Cane Run Power Station
No. 6
277
Louisville Gas & Electric
Paddy Run Power Station
No. 6
65



Minnkota Power Coop.
M.R. Young Station
No. 2
450

PROCESS
STATUS
START-UP DATE
Lime
Operational
8/76
Lime
Operational
12/77
Double Alkali
Contract Awarded
2/79
Lime
Operational
4/73



Fly Ash/Lime
Construction
8/77

REPORTED CAPITAL
COSTS,
$ MILLION
10
12
16.3
3.7



44

$/KW
50
66
58.9
57



98

REPORTED OPERATING
COSTS,
$ ANNUAL
N/A

7.3 MM
905,000





MILLS/KWH
N/A


2.5





COMMENTS
1. The total installed capital cost is an estimated
figure that includes the costs for lime handling and
sludge disposal facilities.
1. The total installed capital cost is an estimated
figure that includes the costs for lime handling and
sludge disposal facilities.
1. The total installed capital cost figure is an estimate
provided by the utility.
2. The annual operating cost figure provided is an
estimate for one year's service following the first
three months of npertions. $4.5 million of this total
will be subsidized by the EPA for technology research,
development and report writing. This, subsidy will not
be utilized for any capital expenditures.
1. The capital cost figures are based on the boiler
rating minus system power consumption. The costs
include everything except the final waste disposal
site. This is a borrow pit supplied by the State
highway department at no cost to the utility.
2. The operating costs provided has been derived by
assuming a 60% unit 60 factor and a 15% fixed charge
factor.
3. Cost of the carbide lime absorbent is confidential.
4. Costs are atypical because the unit is used for
peak loads and the scrubber is a research and
development tool for future full scale installations
now operational, under construction or planned.
1. The total installed capital cost figure represents
an estimated value for the unit's entire emission
control system, including an upstream ESP for pri-
mary parti cul ate control ($12 million).
2. The capital cost figure does not include the ex-
tensive sludge handling and disposal strategy proposed
for this unit (vacuum filters and building, conveyor,
by-pass equipment, trucks and front-end loaders.
Note;  N/A indicates figures are not available.
B-10
                                                                                                                PEDCo ENVIRONMENTAL

-------
                                                  APPENDIX B (Continued).  FGD SYSTEMS ECONOMICS
COMPANY
PLANT
UNITS
TOTAL CAPACITY, HW
Montana Power Co.
Colstrip Plant
Nos. 1 & 2
716


Montana Power Co.
Colstrip Plant
Nos. 3 & 4
Nevada Power Co.
Reid Gardner Station
Nos. 1 & 2
250

Northern Indiana Public Serv.
D.H. Mitchell Station
No. 11
115



PROCESS
STATUS
START-UP DATE
Fly Ash/Lime
Operational
10/75 & 7/76


Fly Ash/Lime
Contract
Awarded
7/80 & 7/81
Sodium Carbonate
Operational
4/74

Well man-Lord
Construction
1977



REPORTED CAPITAL
COSTS,
$ MILLION
32.663


N/A
11

14.825



$/KW
45.32


N/A
44

129



REPORTED OPERATING
COSTS,
$ ANNUAL
1.185 MM


N/A
1.2 MM

6.006 MM



MILLS/KWH
0.26


N/A
N/A

8.1



COMMENTS
1. The total installed capital cost figure is an es-
timated value that includes the venturi scrubbers
installed for paniculate emissions control.
2. The annual operating cost figure is an estimated
value that excludes fixed charges and solid waste
disposal operations.
3. Capital charges were not available to be included
in the figures provided.
4. The cost figures are presented in 1975 and 1976
dollars.
1. Capital cost figures are currently not available for
publication. The contract recently awarded to the
system supplier is expected to exceed $50 MM for both
units.
1. The total installed capital cost figure is an estimate
that was originally provided by the utility for
expenditures completed by installation date (1974).
Included are both scrubbing systems along with all the
raw material handling and pond equipment cost.
2. The annual operating cost figure includes $600,000
annual i zed for each unit.
1. The capital figure includes interest during con-
struction and overhead charges.
2. Reported operating cost figure is a total annualized
cost value that includes:
Operation and maintenance costs.
Anti-oxidant agent costs.
Fixed charges are calculated a 10-15 year plant life-
time (26% of $14,825 MM). Assume an annual unit load
factor of 73.5%.
3. All figures are reported in 1976 dollars.
Note:  N/A indicates figures are not available.
                                                                       B-ll
PEDCo ENVIRONMENTAL

-------
                                                  APPENDIX B (Continued).  FGD SYSTEMS ECONOMICS
COMPANY
PLANT
UNITS
TOTAL CAPACITY, MW
Northern States Power
Sherburne County Generating
Plant
Nos. 1 & 2
1420







Pacific Power & Light
Idaho Power Company
Jim Bridger Plant
No. 3




PROCESS
CTA T( 1C
STATUS
START-UP DATE
Limestone
Operational,
Construction
5/76 & 5/77








Sodium
Contract
Awarded
9/79




REPORTED CAPITAL
COSTS,


$ MILLION
60











50-60 MM








$/KW
44











110-120







REPORTED OPERATING
COSTS,

j
$ ANNUAL
3.77 KM



















MILLS/KWH
0.37






















COMMENTS
1. The total installed capital cost figure includes
direct costs only, indirect costs are excluded.

2. The total cost figure applies to 1975 installation
and does not include escalation factors.
3. The annual operating cost figure includes both
direct and indirect costs for 1976 operations.
4. The $/kW figure is based upon the net generating
capacity of both units (680 Mw/unit, 1360 MW total).
5. The cost of one redundant scrubber train is included.
6. The annual operating cost figure is estimated for
1977 operations at a capacity load factor of 80%.
1. The total installed capital cost figures provided
are estimated values.

2. The system will be comprised of 3 parallel absorp-
tion towers each handling 30.3* of the flue gas
capacity.
3. The reagent, a nominal 30 wt. % Na2C03 purge solu-
tion, will be purchased from a local soda ash
manufacturer.
Note:  N/A Indicates  figures are not available.
                                                                       B-12
                                                                                                                PEDCo  ENVIRONMENTAL

-------
                                                  APPENDIX B (Continued).   F6D SYSTEMS ECONOMICS
COMPANY
PLANT
UNITS
TOTAL CAPACITY, MM
Pennsylvania Power
Bruce Mansfield Plant
Nos. 1 & 2
1670





Philadelphia Electric
Eddystone Generating
Unit No. 1A
316

PROCESS
STATUS
START-UP DATE
Lime
Operational ,
Construction
4/76 & 4/77





Magnesium Oxide
Operational
9/75

REPORTED CAPITAL
COSTS,
$ MILLION
213.200





20.273

$/KW
127.66





64

REPORTED OPERATING
COSTS,
$ ANNUAL
10.344 MM





N/A

MILLS/KWH
2.7





N/A

COMMENTS
1. All cost figures presented are estimates provided
by the utility.
2. The total installed capital cost figure includes
all direct and indirect costs plus escalation
factors .
3. The cost of the venturi scrubbers required for par-
ticulate emission control are included.
4. The cost of one redundant scrubbing train is included.
5. The annual operating cost, calculated in mills/kWh,
is based upon a 90% unit capacity factor.
6. Indirect costs are not included in the annual opera-
ing cost total .
7. All cost figures are reported in 1975 and 1977 dollars.
1. The total installed capital cost figure is a 1972
estimated value, devoid of any escalation factors.
2. Total direct and indirect costs include the three
first stage particulate scrubbers and one second stage
S02 absorber. Also included are the S02 recovery
equipment at the plant, site improvements, and access
roads, engineering and contractor's fees and in-
terest on capital during construction.
3. The costs for the magnesium oxide regenerating
facilities are not Included in the total cost figure.
Note:  N/A Indicates figures are not available.
                                                                                                                     PEDCo ENVIRONMENTAL
                                                                      B-13

-------
                                                  APPENDIX B (Continued).  FGD SYSTEMS ECONOMICS
COMPANY
PLANT
UNITS
TOTAL CAPACITY, MW
Potomac Electric Power
Dickerson Station
No. 3
190

Public Service of New Mexico
San Juan Station
Nos. 1 & 2
715





PROCESS
STATUS
START-UP DATE
Magnesium Oxide
Terminated
9/73

Well man Lord
Construction
7/77





REPORTED CAPITAL
COSTS,
$ MILLION
6.5

89.510





$/KW
68

127.87





REPORTED OPERATING
COSTS,
$ ANNUAL
990,000

7.236 W





NILLS/KWH
N/A

5.0





COMMENTS
1. The total installed capital cost figure is an estimate
provided by the utility in 1973.
2. This figure does not include regeneration and acid
plant costs.
3. The operating cost figure is an estimate provided
for 1974 operations. This figure includes operation
and maintenance costs and acid plant freight and
operation charges. Not included in this figure are
fixed charges, utility charges, project management
and engineering costs.
1. The total installed capital cost figure is an es-
mated value that applies to 1977 installation. In-
cluded are all direct and indirect costs plus an
escalation factor.
2. The $/kW figure is based on a net generating capacity
of 700 MW.
3. The costs of the venturi scrubbers for particulate
removal are included in the total cost figure.
4. The cost of one redundant scrubber train is included.
5. The annual operating costs and the mills/kWh value
derived are estimated for 1978 operations and based
upon a capacity factor of 77%.
6. No credit is allowed for by-product recovery (this
includes both the elemental sulfur product and the
sodium sulfate purge product for use in pulp and paper
processes .
Note:   N/A Indicates figures are not available.
                                                                                                                PEDCo ENVIRONMENTAL
                                                                        B-14

-------
                                                   APPENDIX B  (Continued).  F6D SYSTEMS ECONOMICS
COMPANY
PLANT
UNITS
TOTAL CAPACITY, MW
Rickenbacker AFB
Rickenbacker
Nos. 1 to 7
20

Salt River Project
Coronado Station
Nos. 1 & 2
700 HW
South Carolina Public Service
Wlnyah Generating Station
No. 2
280


Southern Mississippi Power
R.D. Morrow Generating Plant
Nos. 1 & 2
360

PROCESS
STATUS
START-UP DATE
Lime
Operational
3/76

Limestone
Contract
Awarded
4/79 & 4/80
Limestone
Construction


Limestone
Construction
11/77 & 6/78

REPORTED CAPITAL
COSTS,
$ MILLION
2.2

N/A
6.189


18.847

$/KW
110

N/A
24.35


52.35

REPORTED OPERATING
COSTS,
$ ANNUAL
N/A

N/A





MILLS/KWH
N/A

N/A





COMMENTS
1. The total installed capital cost figure includes
adjacent electrical costs, sludge disposal facility
costs, external flue work costs, and other non-
typical equipment costs.
2. Figures are reported in 1976 dollars.
1. The contracts for the ESP and scrubbing system
have just been recently awarded. Actual capital
cost figures have not yet been determined. The
combined cost of these two new power-generating
facilities, including emission control, is estimated
at 685 MM.
1. Fifty percent of the boiler's flue gas will be
scrubbed for S02 removal. SO? removal efficiency is
69%.
2. The total installed capital cost figure is an
estimated value.
3. Total direct and indirect costs for the ESP provided
for primary particulate control upstream of the
scrubbers are included.
4. Sludge handling and disposal facilities, utilities
and services costs, interest on capital during con-
struction, and contractor's fees are not included in
the total installed cost figure.
1. The total installed capital cost figure is an estimate
that applies to 1975 installation dates.
2. Included in the cost figure are the ESP's, scrubbers
and ancillary equipment, fans, construction field
expenses, and interest during construction.
3. Sludge handling and disposal facilities are not In-
cluded in the total cost figure.
Note:  N/A Indicates figures are not available.
                                                                                                                   PEDCo ENVIRONMENTAL
                                                                        B-15

-------
                                                  APPENDIX B (Continued).   FGD SYSTEMS ECONOMICS
COMPANY
PLANT
UNITS
TOTAL CAPACITY, MW
Tennessee Valley Authority
Widows Creek Steam Plant
No. 8
550




Utah Power & Light
Emery Plant
No. 1
400


Utah Power & Light
Hunt ing ton Plant
No. 1
415 MW
PROCESS
STATUS
START-UP DATE
Limestone
construction
3/77




Lime
Letter of Intent
6/78


Lime
Construction
6/77
REPORTED CAPITAL
COSTS,
$ MILLION
56.284




29.0


26
$/KW
102.33




72.5


62.65
REPORTED OPERATING
COSTS,
$ ANNUAL
5.226 K








MILLS/KWH
A 1.72








COMMENTS
1. The total installed capital cost figure is an estimate
that includes all expenditures made by February 1977.
2. Included in the total intalled figure are the costs
of the existing ESP and venturi scrubbers for control
of particulate emissions, plus all direct and in-
direct costs, and escalation.
3. Sludge handling and disposal facilities are not
included in the above estimate.
4. The annual operating cost figure is an estimate that
applies to operation in 1977.
5. The annual operating cost estimate includes par-
ticulate removal costs. Amortization of investment
is not included.
6. The mills/kWh figure derived from is the total annual
cost estimates (direct and indirect) at a unit
capacity facto.- of 63%.
1. The total installed capital cost is a preliminary es-
timate that includes the cost of the scrubbers and
ancillary equipment, lime and sludge handling and dis-
posal equipment.
2. No water is returned to the process from the settling
pond.
3. A part of the flue gas will be by-passed for reheat
requirements.
1. The total installed capital cost is a preliminary
estimate that incldues the cost of the scrubbers and
ancillary equipment, lime handling and sludge hand-
ling and disposal equipment.
Note:   N/A indicates figures are not availabe.
                                                                      B-16
                                                                                                               PEDCo ENVIRONMENTAL

-------
                                                   APPENDIX B (Continued).   FGD  SYSTEMS  ECONOMICS
COMPANY
PLANT
UNITS
TOTAL CAPACITY, MW
Wisconsin Power & Light
Columbia Plant
No. 2
527





PROCESS
STATUS
START-UP DATE
Lime/Limestone
Requesting/
Evaluating
Bids
1/80




REPORTED CAPITAL
COSTS,
$ MILLION
30








$/KW
57








REPORTED OPERATING
COSTS,
$ ANNUAL
4.2 MM








MILLS/KWH









COMMENTS
1. The total installed capital cost figure is a pre-
liminary estimate that includes the scrubbers and
ancillary equipment, erection, disposal piping and
basin area.

2. Sludge handling and disposal equipment and the up-
stream ESP are not included in this figure.
3. The operating cost figures provided are estimated
values.
Note:  N/A indicates figures are not available.
                                                                         B-17
PEDCo ENVIRONMENTAL

-------
B-18

-------
       APPENDIX C

FGD PROCLSS FLOW DIAGRAMS
          C-1
                                PEOCO-ENVIRONMENTAL

-------
C-2

-------
                                               LOUVER
FIVE
                       K39ULC (>)
1




Mi*



















l-
EtC



r-..._






L 1
;a
nf,



>







«S



t n .11








<









|
e





1





















JJ














TACK








0-s

















ST









































-L














^^











..-


\ N




S02 SCKiB3E>
DEXIST£il
[

Jy.1::^""!

I
                                        I	I
                                      1  t
                                          6.5
                                                                                    HOXLE (3)
                      Figure 1.   Choi la No.  1  FGD System:  General Flow Diagram.
                                                    C-3

-------
Figure 2.   Four Corners Prototype  Scrubber  Module:   Cross  Section Diagram.
                                  C-4

-------
            MIST
            ELIMINATOR
   RILEY
VENTRI-SORBER
  SCRUBBER
LIMESTONE
 SLURRY
                                                      A
                                                               ELECTROSTATIC
                                                               PRECIPITATOR
                                         SCRUBBER
                                         I D BOOSTER FAN
                                  PUMP
FLUE GAS
FROM
BOILER
                                                                                             RECYCLE
                                                                                             TO FGD
                                                                   SETTLING POND
           Figure 3.   Simplified  Process  Diagram of  the Duck Creek No.  1 FGD Module.
                                                   C-5

-------
                                                       TO sludge
                                                     treatment plant
Figure  4.   Will County No. 1 FGD  System:  General  Process  Diagram.
                                 C-6

-------
  FLUE
  GAS
 SLURRY
 BLEED
   TO-*-
SETTLING
  POND
                                             REHEATER [~~\
                         MAKEUP
                          WATER
              PEABODY/LURGI
             RADIAL VENTURI
               PEABODY
             SPRAY TOWER
             so "REMOVAL
                                             MIST  ELIMINATOR
z
  PARTICULATE
   REMOVAL
LIMESTONE
  _L
                       SLURRY  HOLD TANK
                                                            WASHWATER
                                                             RECYCLE
                                                               TANK
        Figure 5.   St.  Clair No. 6 FGD System:   General  Process Diagram.
                                      C-7

-------
                              1ST STAGE
                              ADJUSTABLE VENTURI
                              FOR FLY ASH/S02
                                                2ND STAGE
                                                S00 ABSORBER  SCRUBBER
CaS03/S04
FLY ASH SLURRY
            RECYCLE  RETURN  SYSTEM
            TO
      STABILIZATION
        FACILITIES
           Figure 6.   F.  R. Phillips FGD System:   General  Process Diagram.
                                        C-8

-------
                                            NaOH
                                                                                                          FILTRATE
                                                                                                          PUSC?
                                                                                  SLUDGE
                                                                                  BLEND TANK
                                                                          CaSOi;
                                                                        ,  CaC03

                                                                        1       VACUUM'
                                                                               FILTER
CHEMICAL
HJX
XO. I
                                                                          FEEDER
                                                                          SLAKER
                                                                                   LIME FEED
                                                                                     PUMP
  CAUSTIC
  STORAGE TAXS
          SURGE
'<•         TAR*
CARBON
DIOXIDE
STORAGE TANK
                                                     SCRUBBER
                                                     FEED PUMP
                                                                         SODA ASH
                                                                         FEED PUMP
           Figure 7.  General  Motors  Chevrolet Parma  Plant:  General Process Flow  Diagram.
                                                    C-9

-------
                                                                             LIMESTONE
                                                                             SILO
WASTE
DISPOSAL
WASTE
DISPOSAL
MOTHER
LIQUOR
TANK
GYPSUM
          Figuare 8.   Chiyoda  Thoroughbred  101 FGD Prototype:  General Process Diagram.

                                             C-10

-------
                   COAL
                   SUPPLY
                                                 STACK
                                                                •I.D. FAN.
LIMESTONE
SUPPLY
     FEEDER
                                           F.D. FAN
                                                 STACK-GAS-
                                                 SCRUBBER
             PULVERIZER
                                                       RECYCLE
                                                       PUMP
                                                                                               CLARIFIER
    MAKE U?
    WATER

TO ASH DISPOSAL
POND
                 Figure 9.   Hawthorn No.  3 FGD System:   General  Process  Diagram.
                                                 C-ll

-------
                    COAL
                    SUPPLY
                                                    STACK
                                                                    •I.D.  FAN.
LIMESTONE
SUPPLY
     FEEDER
                                                                             STACK GAS
                                                                             REHEATER
                                                 ,AIR HEATER
                                                     DEMISTER
                                                   STACK GAS-
                                                   SCRUBBER
                                                         RECYCLE
                                                         PUMP
                        Figure 10. Hawthorn  No.  4  FGD System:  General Process Diagram.
                                                     C-12
                                                                                                    CLARIFIER
                                                                                                   MAKE UP
                                                                                                   WATER
                                                                                              TO ASH DISPOSAL
                                                                                              POND

-------
Figure 11.   La Cygne No.  1 FGO System:  General Process Diagram.
                             C-13

-------
                                              EXIST. STACK
n
UET
SCRUB
8ER STACK
T\_/T
BY-PASS
DAMPENS
r

_ SCRSJB3ER
A BOOSTER
                                                      V	'
                                                     SPARE
                                        SPARE
                                 SPARE
Figure  12.
Green  River F6D System:  General  Process  Diagram.

                 C-14

-------
Figure 13.   Stock Island Plant FGD System:  Process Flow Diagram.
                             C-15

-------
                       x^7"'
                                                                                «QOtT:-E 
-------
                                                        JTEAH 760'F
                                                            «?« PS:A
                                                            «76.7 IS/KM
Figure  15.   Reid Gardner  FGD  Systems, Units  1, 2, and  3:
                 General Process Diagram.
                            C-17

-------
FLUE GAS
   TO
SCRUBBER

  FIRST
  STAGE
 OOOi
OXIOIZER
                   REHEATER
                     HIST
                   ELIMINATOR
                  OVERFLOW POTS
                   & MARBLE BED
                 REACTION
                   TANK
FLUE  GAS
TO STACK
  RIVER
MAKE-UP
 WATER
                                                             WEIR
                                              THICKENER
                                              UNDERFLOW
                                                PUMP
                                 SPRAY
                                 PUMP  ,
                                                                      ASH POND
                                        LIMESTONE —i
N—


THICKENER


RE
T
i
GIF
AN
f
*C
(
T€?
                                               SLURRY
                                               TA.NK
                                                                                                    SLURRY
                                                                                                     PUMP
                                              ASH POND
                                             RETURN PUMP
         Figure  16.   Sherburne  No.  1  FGD  System:   Simplified  Process  Diagram.
                                               C-18

-------
                                                                     PIPELINES TO RESERVOIR
Figure 17.   Bruce Mansfield No.  1  FGD System:  Simplified Process Diagram.
                                     C-19

-------
                      FRESH
                      WATER -
                      INLET
                         BACKWASH
                         SPRAYS
STACK GAS
FROM I.D.
FANS
PARTICULATE
SCRUBBER
HUMIDIFIED
GAS STREAM
            Mg  (OH)2 SLURRY
PARTICULATE
SCRUBBER
SURGE TANK
               TO  WASTE  WATER
              'TREATMENT SYSTEM
                                                        CLEAN  GAS  OUi^ET
                                      MIST  ELIMINATORS
                                   MIST  ENTRAPMENT  SEPARATOR
               S02 SCRUBBER

               SURGE TANK
                                       VENTURI  ROD  MODULES
                                                                SCRUBBING SLURRY INLET
                                                                    TO Mg S03
                                                                     RECOVERY
    Figure 18.   Eddystone No.  1  FGD System:  General  Process Diagram.
                                  C-20

-------
                                                                             FLUE GAS FRCM
                                                                             7 COAL-FIRED
                                                                             STORES BOILtSS
Figure  19.   Rickenbacker FGD  System:  General Process Diagram.

                               C-21

-------
       I   AIR  >---.

       IFUEL  OIL>—»»] RE HEATER]-- 1
                   \ v  v/
            SCRUBBER\i—lA
                                       •-0--
                                [MAKEUP WATER]
                                                I.D.  FAN
                              SECOND
                               HOLD
                               TANK
SAMPLE POINTS
                                                                                         i	
                                                                                PROCESS
                                                                                 WATER
                                                                                 HOLD
                                                                                 TANK
                                                                                               STACK
                                                                                         ^MAKEUP WATERl
                                                                               DISCHARGE
OGAS COMPOSITION
® PARTICIPATE COMPOSITION  &  LOADING
0 SLURRY OR SOLIDS COMPOSITION
	GAS STREAM
	LIQUOR STREAM
                                                                                             SETTLING POND
                  Figure 20.   Shawnee No.  10  Prototype Test Unit:  General Process Diagram.
                                                   C-22

-------
            AIR
        I FUEL OIL >—>[ REHEATER-— ;
                                                                PROCESS
                                                                 WATER  I
                                                                HOLD TANK
                    SCRUBBER
                    EFFLUENT
                     HOLD
                     TANK
SAMPLE POINTS
OGAS COMPOSITION
®PARTICULATE COMPOSITION & LOADING
©SLURRY OR SOLIDS COMPOSITION
GAS STREAM
LIQUOR STREAM
                                          SETTLING POND
            Figure 21.  Shawnee No. 10 Prototype Test Unit:  General Process Diagram.
                                               C-23

-------
                          FLUE GAS
MAKE-UP WATER
                                  SPRAY TOWER

                  SPRAY TOWER EFFLUENT
                       HOLD TANK
                                                                   VENT   AIR

                                                                     A
                                                       OXIDATION
                                                        TANK
                                                                            CLARIFIED LIQUOR
                                                                                 WATER
                                                                                        D
=>
=»
* A
1
t




_«3 	

1
c
D

	 1 	 t^-
f v_
1
DESUPERSATURATION
TANK
   BLEED  TO
 DEWATERING
^   SYSTEM
                          Figure 21A.   Shawnee No.  10 Prototype  Test Unit:   Modified
                           Mentui/Spray Tovier System for 2-Stage Oxidation Testing.

-------
BOILER
FLUE
GAS
                                                                            SULFUR1C ACID
                                                                            CONTACT ACID
                                                                               PLANT
98% GRADE
                            PUMP
                   Figure  22.   Mystic No.  6  FGD System and  Essex Chemical  Plant
                           Regeneration Facility:  Schematic Flow Diagram.
                                                 C-25

-------
                             SCRUBBED
                                 GAS
                                VACUUM WATER RECOVERY    H?0
Figure 23.   CEA/ADL Dual Alkali  Prototype:   General Process  Diagram.
                                  C-26

-------
                               Off    REGENERATION
                ADSORPTION SECTION

                1.  INLET FLUE
                    GAS DUCTING,  DILUTION AIR
                    DESIGN, AND ADSORPTION
                    SECTION OVERALL LAYOUT.
                2.  ADSORPTION DISCHARGE FANS.
                3.  ADSORBER DISCHARGE FEEDERS
                    CONVEYORS AND SITE GLASSES
                    WHICH SHOW CHAR MOVEMENT.
                4.  ADSORBER FEED CONVEYORS.
                5.  CHAR BUCKET ELEVATORS.
                REGENERATION SECTION

                6.  AIR PREHEATER, SAND
                    FLUID BED HEATER, HOT
                    SAND BUCKET ELEVATOR.
                7.  START UP AIR HEATER.
                8.  SATURATED CHAR SURGE
                    TANK,  SATURATED CHAR
                    FEEDER,  REGENERATOR.
                9.  SAND HEATER BLOWER.
                10.  SAND MAKE UP HOPPER,
                    FEEDER.
                11.  HOT  SAND  CONVEYOR.
                12.  CHAR-SAND SEPARATOR
                    FEEDER.
                13.  REGENERATED CHAR
                    COOLER.
                14.  REGENERATED CHAR
                    BUCKET ELEVATOR, CHAR
                    MAKE UP HOPPER,  FEEDER.
                REDUCTION SECTION
                15.  COAL MAKE UP HOPPER,
                    FEEDER FEED BUCKET
                    ELEVATOR.
                16.  COAL FEED BIN.
                17.  COAL FEED BIN  ACTIVATOR,
                    ROTARY COAL AIRLOCK,
                    RESOX START UP HEATER.
                18.  RESOX REACTOR.
                19. SULFUR CONDENSER, TAIL
                   GAS BLOWER.
               20. CONTROL AIR BLOWER.
               21. ASH DISCHARGE  FEEDER
               22. ASH RECEIVER VESSEL,
                   WEIGH SCALE.
               23. SULFUR STORAGE TANK,
                   SULFUR TRANSFER PUMP.
Figure  24.   FW-BF Dry Adsorption  Prototype:
                                          C-27
General  Equipment  Schematic.

-------
                                                                          CAT-OX MIST
                                                                           ELIMINATOR
  FLUE GAS
FROM EXISTING
   ID FAN
                                                                                          *• STORAGE
                    Figure  25.   Wood River No. 4  Catalytic Oxidation FGD  System:
                                     Simplified Process  Diagram.
                                                C-28

-------
' i    FLUE GAS BY-PASS
 v.i	
                                                                           VENTURI
                                                                      dbi SCRUBBER/ABSORBER
                                     1ST STAGE
                                   ELECTRO-STATIC
                                    PRECIPITATOR
                                                                            TO 2ND
                                                                             STAGE
                                                           MIST
                                                        ELIMINATOR
                     TO DRY ASH HANDLING SYSTEM
                                                                                    DUST COLLECTOR
RECYCLED
POND WATER
                                     TANKCHU-
    -  —/ *  TRANSFER
                                            CRYSTAL
                                             DRYER
 ASH FOND
                            MgO FROM
                           ACID PLANT
                                                         MgS03 TO ACID  PLANT
                          Figure 26.   Dickerson  No. 3 Regenerative FGD System:
                                          General  Process  Diagram.
                                                     C-29

-------
   ALKALI
STORAGE SILO
       SLURRY 8
      MIX TANK
                                       FLUE GAS FROM
                                       PRECIPITATORS
                                        CONTROL
                                        BUILDING
                 THICKENER
         MOTOR  CONTROL

  THICKENER  CENTER
OVERFLOW TANK
                         ABSORBE
                        HOLD TANK
 POWER
', PLANT
 STACK
                    ALKALI
                   MIX TANKS
                                          TURBULENT
                                          CONTACT
                                          ABSORBER
                         Figure 27.  Mohave No. 1 Vertical Test Module:
                                   Simplified Process Diagram.
                                              C-30

-------
                             FOUR SCRUBBER STAGES
                                                                        J
                                                                          I
                                                                                HOT AIR
                                                                                INJECTION
BOOSTER FAN
MIST ELIMINATOR
     Figure 28.   Mohave No.  2 Horizontal  Test  Module:   Simplified  Side  View.
                                      C-31

-------
C-32

-------
APPENDIX 0

DEFINITIONS
  D-l
                         PEOCO-ENVIRONMENTAL

-------
D-2

-------
                                   DEFINITIONS
Boiler Capacity Factor
Boiler Utilization Parameter
Efficiency,
   Particulates
   SO,
FGD Availability Factor
FGD Reliability Factor
FGD Operability Factor
FGD Utilization Factor
FGD Status
   Category 1

   Category 2
   Category 3
 (kWh generation in year)/(maximum continuous generating
capacity in kW x 8760 hr/yr).

Hours boiler operated/hours in period, expressed as a
percentage.
Operational - The actual percentage of particulates re-
moved by the FGD system and the particulate control de-
vices from the untreated flue gas.  All others - The
design efficiency (percentage) of particulate removed by
the FGD system and the particulate control devices.

Operational - The actual percentage of S02 removed from
the flue gas.  All others - The design efficiency.

Hours the FGD system was available for operation  (whether
operated or not)/hours in period, expressed as a percentage.

Hours the FGD system operated/hours FGD system was called
upon to operate, expressed as a percentage.

Hours the FGD system was operated/boiler operating hours
in period, expressed as a percentage.

Hours FGD system operated/hours in period, expressed as
a percentage.
Operational - Unit has been or is in service removing SO-.

Under Construction - Ground has been broken for installa-
tion of FGD system, but FGD system has not become opera-
tional.

Planned, Contract Awarded - Contract has been signed for
purchase of FGD system but ground has not been broken
for installation.

            D-3

-------
                                   DEFINITIONS
   Category 4



   Category 5



   Category 6


   Category 7


FGD Vendor


Fuel Characteristics



Identification Number


New



Operational Experience
Process
Planned, Letter of Intent Signed - Letter of intent has
been signed, but legal contract for purchase has not been
awarded.

Planned, Requesting/Evaluating Bids - Bid requests have
been released but no letter of. intent or contract has
been issued.

Considering only FGD Systems - An FGD system is proposed
as a means to meet an SO- regulation.

Considering an FGD system as well as alternative methods
(Tables 14, 15).

Vendor with a signed contract, letter of intent or strong
commitment because of test unit or past purchases.

Type of fuel, average gross heating value in Btu/lb,
average percent ash and average percent sulfur content
for fuel as fired.

Number of unit in the alphabetical listing in Tables 1,
2, 3 or Tables 14, 15.

FGD unit and boiler were designed at the same time or
space for addition of an FGD unit was reserved when
boiler was constructed.

Operational - Brief summary of FGD system operation
since start-up and description of current month's per-
formance.  All others - Comments regarding state of con-
struction, etc.

Company name if process is patented.  Generic name if
several companies have similar processes.
                                          D-4

-------
                                   DEFINITIONS
Regulatory Class
Retrofit


Sludge Disposal



Start-up Date



Unit Cost
A.   New boiler constructed subject to Federal New Source
     Perforiuancc Standards.

B.   Existing boiler subject to State Standard that is
     more stringent than the Federal New Source Perform-
     ance Standard  (NSPS).

C.   Existing boiler subject to Stats Standard that is
     equal to or less stringent than NSPS.

D.   Other.

E.   Unknown.

FGD unit must be added to an existing bciler not
specifically designed to accommodate FGD unit.

Comments on disposal method for those units generating
sludge including:  lined or unlined ponds, stabilized or
unstabilized sludge, and on- or off-site disposal.

Operational - Date when S02 removal began.  All others -
Date when SO2 removal is scheduled to begin.  Generally
this will be the start-up date of the boiler.

Capital Cost in $/kW including:  S02 absorption and regen-
eration system, S02 recovery system, solids disposal,
site improvements, land, roads, tracks, substation, engi-
neering costs, contractors fee and interest on capital
during construction.

Annualized Cost in mills/kWh including fixed and variable
costs.  Fixed costs include:  interest on capital, deprecia-
tion, insurance, taxes, and labor costs including overhead.
Variable costs include:  raw materials, utilities, and
maintenance.
                                          D-5

-------
                                   DEFINITIONS
Unit Location

Unit Name
Unit Rating
Utility Name
Water Make-Up
City and State listed in mailing address.

Unit identification as it appears in Electrical World -
Direction of Electrical Utilities, McGraw-Hill - Current
Edition - or as indicated by utility representative for
installations in planning stages.

Operational - Maximum continuous gross generation capacity
in MW; Preoperational - maximum continuous design genera-
tion capacity in MW.

Name of corporation as it appears in Electrical World -
E/irectory of Electrical Utilities, McGraw-Hill - Current
Edition - as space permits.
Gallons per
capacity.
minute of make-up water required per MW of
                                          D-6

-------