SUMMARY REPORT - FLUE GAS DESULFURIZATION SYSTEMS -  MAY - JUNE  1977
                                                                          PAGE
TABLL
  1   SUMMARY LIST OF FGD SYSTEMS
  2   STATUS OF FGD SYSTEMS
  3   SUMMARY LIST OF FGD SYSTEMS IN THE EARLY PLANNING STAGES
  H   STATUS OF FGD SYSTEMS IN THE EARLY PLANNING STAGES
  5   PERFORMANCE DESCRIPTION FOR OPERATIONAL FGD SYSTEMS
  6   NUMBER AND TOTAL MW OF FGD SYSTEMS
  7   SUMMARY OF FGD SYSTEMS BY COMPANY
  8   SUMMARY CF FGD SYSTEMS BY VENDOR
  9   SUMMARY OF NEW AND RETROFIT FGD SYSTEMS BY PROCESS
 10   SUMMARY OF OPERATING FGD SYSTEMS BY PROCESS AND GENERATING UNITS
 11   SUMMARY CF SLUDGE DISPOSAL PRACTICES FOR OPERATIONAL FGD SYSTEMS
 12   SUMMARY OF FGD SYSTEMS BY PROCESS AND REGULATORY CLASS
 13   SUMMARY OF OPERATIONAL FGD SYSTEMS
 1**   SUMMARY OF FGD SYSTEMS UNDER CONSTRUCTION
 15   SUMMARY OF PLANNED FGD SYSTEMS
 16   FGD SYSTEM OPERATIONS THAT HAVE BEEN TERMINATED OR SHUT DOWN INDEFINITELY
 17   TOTAL OF FGD MEGAWATT CAPACITY BY YEAR                                            311
      FGD SYSTEMS ECONOMICS                                                     APPENDIX  A
      FGD PROCESS FLOW DIAGRAMS                                                 APPENDIX  B
      DEFINITIONS                                                               APPENDIX  C
                                                                              3
                                                                              9
                                                                             35
                                                                             39
                                                                             <*5
                                                                            201
                                                                            205
                                                                            209
                                                                            213
                                                                            217
                                                                            221
                                                                            225
                                                                            231
                                                                            235
                                                                            239
       PREPARED BY
PEDCO ENVIRONMENTAL INC.
     11**99 CHESTER ROAD
 CINCINNATI. OHIO  <*52«*6
                                                    PREPARED FOR
                                      DIVISION OF STATIONARY SOURCE ENFORCEMENT
                                                         AND
                                     INDUSTRIAL ENVIRONMENTAL  RESEARCH  LABORATORY
                                        U.S. ENVIRONMENTAL PROTECTION AGENCY
                                                 RESEARCH TRIANGLE PARKt
                                                  NORTH  CAROLNA   27711
                       CONTRACT NO. 66 •
                             TASK NO. 3

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  July  12,  1977
PEDCo  ENVIRONMENTAL
                11.499 CHESTER ROAD
             CINCINNATI. OHIO 4524.6
                     (513) 782--47OO
  Enclosed  is  a copy of the April-May 1977 report titled, The
  Status  of Flue Gas Desulfurization Systems in the United
  States.   This report is prepared every other month by PEDCo
  Environmental, Inc., under a contract to the Industrial
  Environmental Research Laboratory/RTF and the Division of
  Stationary Source Enforcement of the U.S. Environmental
  Protection Agency.  Table I, listed below, summarizes the
  current status of these systems.

                              Table I

                NUMBER AND TOTAL MW OF FGD SYSTEMS
Status
Operational
Under construction
Planning
Contract awarded
Letter of intent
Requesting/evaluating bids
Considering only FGD systems
TOTAL
NO. Of
units
27
29

20
5
5
33
119
MW
7,319
12,648

9,797
1,892
3,565
14,856
50,077
  Table  II  gives the categorized breakdown for FGD units,
  comparing the May report totals with those of the March
  report.

  Table  III summarizes the individual units that changed
  status during the report period.
                                BRANCH OFFICES
CHESTER TOWERS
                         Crown Center
                        Kansas City. Mo.
       Professional Village
        Chapel Hill. M.C.

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                          Table II

             NUMBER AND TOTAL MW OF FGD SYSTEMS

            MAY REPORT VERSUS MARCH REPORT PERIOD

Status
Operational
Under construction
Planning
Total
April-May
1977
No. of
units
27
29
63
119

MW
7,819
12,648
30,110
50,077
January-February-March
1977
No. of
units
24
33
62
119

MW
5,997
13,918
29,775
49,690
The performance of the operating systems is summarized in
Table IV.  Other activity highlights during the months of
April and May are outlined below:

Arizona Public Service reported the following items in
connection with the utility's FGD installations:

     0    Cholla No. 1 remained in service throughout the
          report period.  The average system reliability
          index values for the months of April and May were
          100 percent and 87 percent, respectively.  The
          unit was brought down during the month of May for
          a scheduled mid-year cleanout and minor repair
          work.

     0    Construction of Cholla No. 2 is still in progress
          and on schedule.  Start-up is scheduled for June
          1978.

     0    Cholla No. 4, a 350-MW, coal-fired, power-generating
          unit, is currently under construction.  APS is now
          in the preliminary design stage for the inclusion
          of an FGD system on this unit.  The SO2 emission
          regulations, scrubbing process, and system supplier
          have not been determined.

Central Illinois Light Company reported that the experimental
operations of the scrubber module at Duck Creek have been
terminated.  The 100-MW equivalent ventri-sorber module,
supplied by Riley Stoker/Environeering, was taken out of the
gas stream April 1, 1977, after approximately 9 months of
experimental operations.  This module is the first of four
modules designed to treat the flue gas resulting from the
combustion of high-sulfur Illinois coal in a 400-MW steam
boiler.  All four modules will be brought on line in August

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1978 for full-scale integrated operations.  During the
interim, Duck Creek No. 1 will remain in commercial service,
firing low sulfur  (0.6 percent) Colorado coal.  Particulate
matter removal is being achieved by two parallel electrostatic
precipitators installed upstream of the scrubber plant.

Central Illinois Public Service Company reported that con-
struction of the double alkali scrubbing facility at the
Newton Station is approximately 15 percent complete.  This
sodium-calcium double alkali scrubbing system is supplied by
Buell-Envirotech and designed to treat flue gas resulting
from the combustion of high sulfur (4 percent), high chloride
(0.2 percent) coal in a 575-MW boiler.  The start-up date
for the No. 1 unit has been delayed to November 1979.  The
utility cites problems with financing, cash flow, and an
unprecedented scrubber plant design as the major causes for
the start-up delay.

Cincinnati Gas and Electric reported that bids are still
being evaluated for a scrubber plant planned for the 600-MW
rated No. 2 unit at the East Bend Station.  A process,
system supplier, and a coal type and source have not been
determined.  The No. 2 unit start-up date is January 1981.

Colorado-Ute Electric Assn. reported that a contract in ex-
cess of $60 million has been awarded to Peabody Engineered
Systems for two limestone slurry spray tower scrubbing sys-
tems for installation on two 450-MW coal-fired power-generating
units at the Craig station.  The start-up date for the
operation of both scrubber plants is March 1979.

Columbus and Southern Ohio Electric (C&SOE) reported that
the B-side TCA module on Convesville No. 5 was in service
during the report period, operating 261 hours in April and
355 hours in May.  Problems encountered in FGD operations
were as follows:  an abundance of scrap rocks and metal in
the lime supply, rubber lining peeling in the absorber
(C&SOE has determined the peeling problem to be an application
problem), and continuing stack liner failure.  Preliminary
tests indicate SO2 removal of greater than 90 percent.  The
replacement A-side TCA module will be available for commercial
service in January 1978.

Commonwealth Edison reported that experimental scrubber
operations at the Will County Station continued during the
months of April and May.  During the period, a number of
scrubber characterization and component evaluation studies
were conducted.  Specifically, a high sulfur coal sludge
study, conducted by the utility and UOP, and a magnesium
oxide innoculation and forced oxidation study, also conducted
by the utility, were completed during the period.  In addition,
an SO2 analyzer was also evaluated for performance and
reliability characteristics.

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Duquesne Light reported the following items in connection
with the utility's FGD installations:

     0    The Elrama Station continued operations with flue
          gas from two boilers being discharged into the
          five module-single-stage scrubber plant.  Con-
          struction of the two additional 120-foot diameter
          thickeners continued during the period.  In addi-
          tion, the utility also reported that the rubber-
          lined recycle pump evaluation study has been ter-
          minated because of severe corrosion and gouging.
          Full compliance plant operations are scheduled to
          commence sometime during the early part of 1978.

     0    The scrubber plant at the F.R. Phillips Station
          was in service and available 75 percent during the
          report period.  The interim IOCS sludge stabliza-
          tion facility remained in service during the
          period.  Construction of the permanent IOCS stabi-
          lization complex is continuing and will be ready
          for full-compliance plant operations scheduled for
          December 1978.   The Carborundum impeller and wear
          ring recycle pump evaluation study also continued
          during the period,  bringing total operating time
          to in excess of 5000 hours of problem-free operations

The Kansas City Power and Light Co.  reported the following
items concerning the utility's FGD installations.

     0    The Hawthorn No.  3  and No.  4 scrubbing systems
          were in service during the report period,  operating
          408 hours and 311 hours,  respectively,  in  April
          and 302 hours and 180 hours, respectively,  in May.
          The system operability values for the No.  3 unit
          were 57 and 58 percent for the months of April and
          May, respectively.   Unit No. 4 FGD system  operability
          values for the same period were 43 and 54  percent,
          respectively.  Low systems'  demand during  the
          month of May was caused by a natural gas supply
          availability.  The operability index values shown
          above are calculated only for coal-fired operations.

     0    The total system availability index value  for the
          La Cygne No. 1 scrubber plant was approximately 93
          percent for the month of April.   Turbine problems
          forced the unit out of service for the month of
          May.  The eighth scrubber module was in service
          for a short period during the month of April.   The
          unit is expected to be back in service during the
          latter part of June with all eight modules  in the
          flue gas stream.

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Kansas Power and Light reported that Lawrence No. 4 fired
natural gas during the report period, thus requiring no
scrubber plant operations.  The original limestone injection
and tail-end scrubbing system installed on Lawrence No. 5 in
1971 has been and still is in service, removing fly ash and
sulfur dioxide from coal-fired flue gas.  Adjacent to the
original scrubber installation, a new rod section and spray
tower absorber system is being constructed.  This wet lime-
stone scrubbing system consists of two large rod section and
spray tower absorber modules, each module capable of handling
50 percent of the flue gas from the boiler.  The original
system will remain in service until the new system is com-
pleted and cut into the gas path in March 1978.

Kentucky Utilities reported that the Green River FGD system
was in service during the April-May period, treating flue
gas from two of the three boilers ducted into the FGD sys-
tem.  Scrubber service times for the months of April and May
were 164 and 513 hours, respectively.  The system's avail-
ability, operability, reliability, and utilization index
values for the month of April were 40, 98, 98, and 23 per-
cent, respectively.  The May values were 99, 98, 98, and 69
percent, respectively.

Louisville Gas and Electric reported the following items
concerning the utility's FGD installations:

     0    The 178-MW Cane Run No. 4 scrubber plant ran for
          the first 18 days of April with a reliability in-
          dex value of 94 percent.  At that time, the unit
          was shutdown for extensive modifications scheduled
          to last through July 12.  Modifications include
          increasing the liquid-to-gas ratio by the addition
          of a new spray header, replacing the centrifugal
          demister with a Chevron demister, the installation
          of direct-fired oil reheat designed for AT = 50°F,
          replacing the Carboline liner from the demister to
          the stack with Plasite 4005, and the installation
          of a Precrete stack liner.

     0    The 65-MW Paddy's Run No. 6 lime-based scrubbing
          plant operated through mid-April demonstrating an
          operability index value of 95 percent.  During the
          remainder of the report period, the scrubber was
          shutdown because the scrubber operations crew was
          temporarily assigned to boiler operations.  The
          re-start of scrubber operations was scheduled for
          late-June. Preliminary results of the high-calcium,
          virgin lime scrubber/sludge characterization study
          indicate that SO2 removals greater than 99.5
          percent can be obtained with the addition of
          magnesium hydroxide to the scrubbing slurry.

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Minnesota Power and Light Company announced that it has
signed a letter-of-intent with Peabody Engineering for a
lime/alkaline fly ash FGD system at the 500-MW Clay Boswell
No. 4 plant.  The spray tower absorbers will be designed to
remove 89 percent of the inlet SO2-  The Combustion-Engineering
boiler will fire low-sulfur Colstrip coal with a sulfur con-
tent of 0.8 percent.

Minnkota Power reported that construction of the Milton R.
Young No. 2 scrubber plant is approximately 90 percent
complete and that start-up is still planned for August 1977.
This system is designed to treat flue gas from the 450-MW
steam boiler, using the fly ash collected in the electrostatic
precipitators as the principal source of SO2 absorbent.
Commercial lime will supplement the natural alkali ash
supply when necessary.

Nevada Power provided the following general information for
the Reid Gardner FGD systems:

     0    The Reid Gardner No. 1 scrubber plant remained out
          of service throughout the entire report period be-
          cause of on-going repairs to the scrubber liner.
          Damage was caused by an air preheater malfunction.

     0    The Reid Gardner No. 2 scrubber plant was operating
          during the entire report period except for a two-
          week outage for boiler maintenance.

     0    The Reid Gardner No. 3 scrubber system operated
          with no problems during April, but was down from
          May 1 to May 21 for the replacement of the FRP
          liner in the separator.

Northern Indiana Public Service Company announced that ini-
tial scrubber operations have commenced at the D.H. Mitchell
No. 11 unit.  The Wellman-Lord SC>2 recovery system first
operated June 13 and the Allied SC>2 reduction unit first
operated June 15, thereby achieving integrated mode opera-
tions.  Unit No. 11 will operate at a reduced rating of 70
to 75 MW until June 27 at which time it will go down for
final repairs to the preheater.  Subsequent to these repairs,
the utility plans to begin a 16-day acceptance test in early
July.

Northern States Power reported the following items concerning
the utility's FGD activities:

      0    Sherburne No. 1 was in service during the report
          period until May 14 at which time it was taken
          off-line for major turbine overhaul.  The C-E
          marble bed absorber system demonstrated an avail-
          ability index of 95 percent during April and 92
          percent for the first 13 days in May.  The unit
          was scheduled for re-start on June 19.

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     0    Sherburne No. 2 scrubber operations began April 1.
          The emissions control system is currently undergoing
          performance testing.  During April, the No. 2
          scrubber system demonstrated a 92 percent availability
          and for May, the availability index was 91 percent.
          The first two months of operations have been
          relatively problem-free.

Pennsylvania Power reported that it is in the process of
rewriting the Bruce Mansfield No. 1 file for the FGD summary
report and that this updated information will be available
for the next report period.

Philadelphia Electric Company reported that Mag-Ox FGD
operations were re-started at Eddystone Unit No. 1A in May
on a noncontinuous basis.  During May, the system operated
206 hours, representing a utilization index value of 28
percent.  Currently, only one of the two available ventri-
rod beds is being used for SO2 removal.  No removal efficiencies
had been measured as of the end of the report period.  The
first MgSC«3 regeneration operations were schedule for late
June at the Essex Chemical plant.

Springfield City Utilities reported the start-up of scrubbing
operations at the Southwest Station for Unit No. 1, a new
20Q-MW coal-fired power-gtnerating unit.  System start-up
occurred at 2:00 a.m. on April 6.  Subsequent operations
through the report period were intermittent as attempts were
made to rectify varous start-up related problems.  Boiler
related problems, specifically in the air heater, have
caused very high excess air requirements and contributed to
the delay of full-scale, continuous scrubber operations.

The South Carolina Public Service Authority reported a tem-
porary delay in the start-up of power generating and S02 re-
moval operations at the 280-MW Winyah Unit No. 2.  All
equipment is on-site, installed, and ready for start-up with
the exception of three relays.  Delivery is expected at any
time and subsequent to installation all systems will commence
operations.

The Bechtel Corporation reported that experimental work
continued at the Shawnee TVA/EPA Alkali Scrubbing Test
Facility through March, but a scheduled 2-month boiler
maintenance outage curtailed testing through April and May.
During March, forced oxidation tests in the lime scrubbing
mode  (venturi/spray tower prototype) greatly enhanced solids
settling rates and filter cake solids content.  In addition,
limestone type and grind tests (TCA prototype) indicated
improved SO2 removal with the use of finer ground limestone.

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Tennessee Valley Authority announced the start-up of scrubber
operations at its 550-MW Widow's Creek Unit No. 8, in Bridgeport,
Alabama.  Start-up and shakedown procedures began on April
30.  Commercial operation for the four-train limestone SO2
removal system is anticipated by the end of summer.

Utah Power and Light Company reported the following items
regarding its FGD installations:

     0    Construction has begun at the 400-MW Emery No. 1
          installation in Emery County, Utah.  SO2 removal
          will be effected by a Chemico pebble lime wet
          scrubbing system.

     0    At the 415-MW Huntington No. 1 unit, the start-up
          of scrubbing operations has been delayed from June
          1977 until December 1977.

Wisconsin Power and Light has signed a letter-of-intent with
Chemico to design and supply an SO2 control system for the
527-MW Columbia No. 2 unit.  The control system will utilize
a lime/alkaline fly ash absorbent in spray tower absorber
modules.  Current plans include SO2 removal from 60 percent
of the flue gas as opposed to the original 50 percent.  Re-
heat will be provided by the 40 percent of the flue gas
which is bypassed around the scrubber plant.

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Table III.  SUMMARY OF CHANGES:  FGD SUMMARY REPORT,




                  APRIL - MAY 1977
FGD status report
3/31/77
Alabama Electric Power Co -Op
Tomb ig bee No. 3
Arizona Public Service
Choi la No. 4
Arizona Public Service
Four Corners No. S
Central Illinois Light Co.
Duck Creek No. 1A
Central Illinois Light Co,
Duck Creek No. 1
Colorado- UTE
Craig Mo. 1
Craig No. 2
Gulf Power Co.
Scholz No. IB and 2B
Kansas Power and Light Co.
Lawrence No. 5
Minnesota Power and Light Co.
Clay Boswell No. 4
Northern Indiana Public Service
Co.
Mitchell No. 11
Northern States power Co.
Sherburne No. 2
Springfield City Utilities
Southwest No. 1
Tennessee Valley Authority
Widow's Creek No. 8
Utah Power and Light Co.
Emergy No. 1
Wisconsin Power and Light Co.
Columbia No. 2
5/31/77
Operational
No.
24



-1


-1
+1

+ 1
+1
•fl
+1


27
MW
5,997



100


23
400

115
680
200
550


7,819
Under
construction
No.
33
-1








-1
-1
-1
-1
•H

29
MW
13,918
225



100




115
680
200
550
400

12,648
Contract
awarded
No.
18
+ 1




+ 1
+1







-1

20
MW
9,072
225




450
450







400

9,797
Letter of
intent
No.
3








4-1





+ 1
5
MW
865








500





527
1,892
Requesting/
evaluation
bids
No.
9





-1
-1


-1





-1
5
MW
5,492





450
450


500





527
3,565
Considering
PGD
No.
32

+ 1













31
MW
14,346

350
160












14,856
Total
No.
119

tl

-1


-1
+1







119
MW
49,690

350
160
100


23








50,077

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Table  IV.    PERFORMANCE  OF  OPERATIONAL  UNITS  DURING  APRIL  - MAY PERIOD
Plant
Cholla 1
Coneeville 5
Will County 1
Elrasia
Phillips
Hawthorn 3
Hawthorn 4
La Cygne
Lawrence 4
Lawrence 5
Green River
1, 2, ind )
Cane Run
Paddys Run
Colstrip 1
Colstrip 2
Reid Gardner 1
Reid Gardner 2
Reid Gardner }
D.H. Mitchell 11
Sherburne 1
Sherburne 2
Bruce
Mantfield 1
Eddystone 1A
Southwest 1
Shavnee 10A
shavrnee 1 08
Widow's Creek 8
Total (27)
FGD system
denqn
capacity
115
400
167
510
410
140
100
820
US
400
64
lit
6S
360
360
125
12S
125
115
710
680
8J5
120
200
10
10
550
7B19
FGD unit
on-1 me
during
per iod*
115
200
167
200
410
HO
100
820

400
43
178
65



125
129
70
710
680

120
200


275
614}
NO
infornat ion
for this
period













360
)«0






835





1555
Shut down
throughout
period

200

310




125

21




12S


45





10
10
275
1121
FGD lystem
avail-
ability («)••
April

42
66

75


93


40

98






95
92







May

58
94

75





99








12
91







FGD systen
op«ra-
bility (»)••
Apr 1 1
99
40
49


57
43



98
95
















H»y
87
48
27


58
54



98

















FGD system
reliability
[«)"
April
100
41








98

















May
87
51








98

















FGD syaten
utilization
(%!*•
April

37
41







23

















May

50
25







69

















            * Thi. category include* the flue ?as capacity beinf handled by the FCD iyeten at least part of the Um>
             the report period,
           " The percent figures listed sre average values for sll the system scrubbing trains during the period in
                                                                                        during

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         TABLE   1

SUMMARY LIST  OF  FGD SYSTEMS
                                                               oo
                                                               CO
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                                                               CO
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                                   PEDCo  ENVIRONMENTAL
                                         CINCINNATI. OHIO 45246

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                                          TABLE 1
                               SUMMARY LIST OF FGD SYSTEMS
   FGO  STATUS REPORT 06/77

   I.D. NUMBER AND COMPANY NAME
        UNIT NAME
            LOCATION
START UP DATE   STATUS
                                                                                                                          RE6
                                                                                                                          CLASS
    1 ALABAMA ELECTRIC COOP
    2 ALABAMA ELECTRIC COOP
    3 ALLEGHENY POWER SYSTEM
    »' ALLEGHENY POWER SYSTEM
    5 ARIZONA ELECTRIC POWER COOP
    6 ARIZONA ELECTRIC POWER COOP
    7 ARIZONA PUBLIC SERVICE
    8 ARIZONA PUBLIC SERVICE
    9 ARIZONA PUBLIC SERVICE
   10 ARIZONA PUBLIC SERVICE
   11 ARIZONA PUBLIC SERVICE
   12 BASIN ELECTRIC POWER COOP
   13 BASIN ELECTRIC POWER COOP
   1H BASIN ELECTRIC POWER COOP
   15 BASIN ELECTRIC POWER COOP
   16 BASIN ELECTRIC POWER COOP
   17 B^S RIVERS ELECTRIC COOP CORP.
   18 BUZOS ELECTRIC POWER COOP
   19 CENTRAL ILLINOIS LIGHT CO.
   20 CENTRAL ILLINOIS LIGHT CO.
   21 CENTRAL ILLINOIS PUBLIC SERV
   22 CINCINNATI GAS X ELECTRIC CO.
   23 COLORADO UTE ELECTRIC ASSN.
   2H COLORADO UTE ELECTRIC ASSN.
   25 COLUMBUS X SOUTHERN OHIO ELEC.
   26 COLUMBUS s SOUTHERN OHIO ELEC.
   27 COLUMBUS A SOUTHERN OHIO ELEC.
   28 COLUMBUS X SOUTHERN OHIO ELEC.
   29 COMMONWEALTH EDISON
   30 COMMONWEALTH EDISON
   31 DUOUESNE LIGHT
   32 OUOUESNE LIGHT
   33 EASTERN KENTUCKY POWER COOP
   3«» INDIANAPOLIS POWER X LIGHT CO.
   35 INDIANAPOLIS POWER X LIGHT CO.
     TOMBIGBEE NO. 2
     TOMBIGBEE NO. 3
     PLEASANTS NO. 1
     PLEASANTS NO. 2
     APACHE NO 2
     APACHE NO 3
     CHOLLA NO 1
     CHOLLA NO 2
     CHOLLA NO. H
     FOUR CORNERS NO. H
     FOUR CORNERS NO. SB
     ANTELOPE VALLEY NO. 1
     ANTELOPE VALLEY NO. 2
     LARAMIE RIVER NO. 1
     LARAMIE RIVER NO. 2
     LARAMIE KIVER NO. 3
     REID NO. 2
     ATACOSA MCMULLEN NO. 1
     DUCK CREEK NO. 1
     DUCK CREEK NO.2
     NEWTON NO.l
     EAST BEND NO 2
     CRAIG NO. 1
     CRAIG NO. 2
     CONESVILLE NO 5
     CONESVILLE NO 6
     POSTON NO. 5
     POSTON NO. 6
     POWERTON NO. 51
     WILL COUNTY NO 1
     ELRAMA POWER STATION
     PHILLIPS POWER STATION
     SPURLOCK GENERATING PLANT
     PETERSBURG NO 3
     PETERSBURG NO t
     JACKSON ALABAMA
     JACKSON ALABAMA
     BELLMONT W VIRGINIA
     BELLMONT W VIRGINIA
     COCHISE ARIZONA
     COCHISE ARIZONA
     JOSEPH CITY ARIZONA
     JOSEPH CITY ARIZONA
     JOSEPH CITY ARIZONA
     FARMINGTON NEW MEXICO
     FARMINGTON NEW MEXICO
     BEULAH  NORTH DAKOTA
     BEULAH  NORTH DAKOTA
     WHEATLAND WYOMING
     WHEATLANO WYOMING
     WHEATLAND WYOMING
     SEBREE KENTUCKY
     SAN MIGUEL  TEXAS
     CANTON ILLINOIS
     CANTON ILLINOIS
     NEWTON ILLINOIS
     RABBIT HASH KENTUCKY
     CRAIG COLORADO
     CRAIG COLORADO
     CONESVILLE OHIO
     CONESVILLE OHIO
     ATHENS OHIO
     ATHENS OHIO
     PEKIN  ILLINOIS
     ROMEOVILLE ILLINOIS
     ELRAMA PENNSYLVANIA
     SOUTH HEIGHT PENNSYLVANIA
NO.2 MAYSVILLE KENTUCKY
     PETERSBURG INDIANA
     PETERSBURG INDIANA
1.  OPERATIONAL UNITS
2*  UNITS UNDER CONSTRUCTION
3.  PLANNED - CONTRACT AWARDED
<*.  PLANNED - LETTER OF INTENT SIGNED
5*  PLANNED " REQUESTING/EVALUATING BIOS
6.  CONSIDERING ONLY FGD SYSTEMS
A.  BOILER CONSTRUCTED SUBJECT TO FEDERAL NSPS
B,  BOILER SUBJECT To STATE STANDARD THAT IS MORE STRINGENT THAN THE FEDERAL NSPS
C.  BOILER SUBJECT TO STATE STANUAKQ THAT IS EQUAL TO OR LESS STRINGENT THAN NSPS
D.  OTHER
E.  REGULATORY CLASS UNKNOWN
       6.78
       6-79
       3-79
       3-80
       6-78
       *-79
      10-73
       6-78
       6-80
       0- 0
       0- 0
       0-81
       0-83
       *-80
      10-80
       6-83
      12-79
      12-79
       8-78
       1-82
      11-79
       1-81
       3-79
       3-79
       2-77
       1-78
       0-81
       0-83
      12-79
       2-72
      10-75
       7-73
       3-80
       9-77
       
-------
                                          TABLE 1
                               SUMMARY LIST OF FGD SYSTEMS
  FGD STATUS REPORT 06/77

  1.0. NUMBER AND COMPANY NAME
                                     UNIT NAME
                                                                        LOCATION
                                                            START UP DATE   STATUS
                                                      REG
                                                      CLASS
   36 KANSAS CITY POWER
   37 KANSAS CITY POWER
                       LIGHT
                     * LIGHT
38 KANSAS CITY POWER * LIGHT
39 KANSAS POWER & LIGHT
40 KANSAS POWER ft LIGHT
41 KANSAS POWER ft LIGHT
42 KANSAS POWER ft LIGHT

-------
                                          TABLE  1
                               SUMMARY  LIST  OF FGO  SYSTEMS
  FGO STATUS REPORT 06/77

  1.0. NUMBER AND COMPANY NAME
    UNIT NAME
       LOCATION
                                                             START  UP  DATE   STATUS
                   RE6
                   CLASS
   71 NORTHERN INDIANA PUB SERVICE
   72 NORTHERN INDIANA PUB SERVICE
   73 NORTHERN STATES POWER CO.
   7* NORTHERN STATES POWER CO.
   75 NORTHERN STATES POWER CO.
   76 NORTHERN STATES POWER CO.
   77 OTTER TAIL POWER COMPANY
   76 PACIFIC POWER AND LIGHT CO.
   79 PENNSYLVANIA POWER CO*
   80 PENNSYLVANIA POWER CO.
   81 PENNSYLVANIA POWER CO.
   82 PHILADELPHIA ELECTRIC CO.
   83 PHILADELPHIA ELECTRIC CO.
   81 PHILADELPHIA ELECTRIC CO.
   85 PHILADELPHIA ELECTRIC CO.
   86 POTOMAC ELECTRIC ft POWER
   87 POTOMAC ELECTRIC ft POWER
   88 PUBLIC SERVICE CO OF NEW MEX.
   89 PUBLIC SERVICE CO OF NEW MEX.
   90 PUBLIC SERVICE CO OF NEW MEX.
   91 PUBLIC SERVICE CO OF NEW MEX.
   92 PUBLIC SERVICE OF INDIANA
   93 PUBLIC SERVICE OF INDIANA
   91 SALT RIVEK PROJECT
   95 SALT RIVER PROJECT
   96 SALT RIVER PROJECT
   97 SOUTH CAROLINA PUBLIC SERVICE
   98 SOUTHERN ILLINOIS POWER CO OP
   99 SOUTHERN INDIANA GASXELECTRIC
  100 SOUTHERN MISSISSIPPI ELECTRIC
  101 SOUTHERN MISSISSIPPI ELECTRIC
  102 SPRINGFIELD CITY UTILITIES
  103 TENNESSEE VALLEY AUTHORITY
  101 TENNESSEE VALLEY AUTHORITY
  105 TENNESSEE VALLEY AUTHORITY
1.  OPERATIONAL UNITS           1.
2.  UNITS UNDER CONSTRUCTION    5.
3.  PLANNED - CONTRACT AWARDED  6.
 BAILLY NO.  8
 D.H.  MITCHELL NO.11
 SHERBURNE COUNTY STATION NO.l
 SHERBURNE COUNTY STATION NO.2
 SHERBURNE COUNTY STATION NO.3
 SHERBURNE COUNTY STATION N0.i»
 COYOTE NO.  1
 JIM BRIDGER NO.  1
 BRUCE MANSFIELD  NO.  1
 BRUCE MANSFIELD  NO.  2
 BRUCE MANSFIELD_NO.  3
 CROHBY
 EODYSTONE NO. lA
 EDOYSTONE NO. IB
 EDDYSTONE NO. 2
 DICKERSON NO.l
 DICKERSON NO.2
 SAN JUAN NO. 1
 SAN JUAN NO. 2
 SAN JUAN NO. 3
 SAN JUAN NO. 1
 GIBSON NO.  3
 GIBSON NO.  1
 CORONADO NO.l
 CORONADO NO.2
 CORONAOO NO.3
 WINYAH NO.  2
 MARION NO.  1
 A.B.  BROWN NO.l
 R.O.  MORROW NO.l
 R.D.  MORROW NO.2
 SOUTHWEST NO. 1
 SHAWNEE N0.10A
 SHAWNEE N0.10B
 WIDOWS CREEK NO. 8
CHESTERTON INDIANA
GARY INDIANA
bECKER MINNESOTA
BECKER MINNESOTA
BECKER MINNESOTA
BECKER MINNESOTA
BEULAH NORTH DAKOTA
ROCK SPRINGS WYOMING
SHIPPIN6PORT PENNSYLVANIA
SHIPPINGPORT PENNSYLVANIA
SHIPPINGPORT PENNSYLVANIA
PHOENIXVILLE PENNSYLVANIA
EDDYSTONE PENNSYLVANIA
EODYSTONE PENNSYLVANIA
EDDYSTONE PENNSYLVANIA
OICKERSON  MARYLAND
DICKERSON  MARYLAND
WATERFLOW NEW MEXICO
WATERFLOW NEW MEXICO
WATERFLOW NEW MEXICO
WATERFLOW NEW MEXICO
GIBSON COUNTY INDIANA
GIBSON COUNTY INDIANA
ST. JOHNS ARIZONA
ST. JOHNS ARIZONA
ST. JOHNS ARIZONA
GEORGETOWN SOUTH CAROLINA
MARION  ILLINOIS
WEST FRANKLIN INDIANA
HATTIESBURG MISSISSIPPI
HATTIESBURG MISSISSIPPI
SPRINGFIELD MISSOURI
PAOUCAH KENTUCKY
PADUCAH KENTUCKY
BRIDGEPORT ALABAMA
PLANNED - LETTER OF INTENT SIGNED
PLANNED - REQUESTING/EVALUATING BIOS
CONSIDERING ONLY FGD SYSTEMS
A.  BOILER CONSTRUCTED SUBJECT TO FEDERAL NSPS
B.  BOILER SUBJECT TO STATE STANDARD THAT IS MORE STRINGENT THAN THE FEDERAL NSPS
C.  BOILER SUBJECT To STATE STANDARD THAT IS EQUAL TO OR LESS STRINGENT THAN NSPS
D.  OTHER
E.  REGULATORY CLASS UNKNOWN
 0- 0
 6-77
 3-76
 1-77
 5-81
 5-83
 5-81
 9-79
 1-76
10-77
 1-80
 6-60
 9-75
 6-80
 6-60
 0-78
 0-76
11-77
11-77
 1-79
 5-61
 0-76
 0-79
 1-79
 1-60
 0-87
 7-77
 6-76
 1-79
11-77
 8-78
 1-77
 1-72
 1-72
 5-77
6
1
1
1
5
5
6
3
1
2
3
6
1
1
6
6
6
2
2
1
6
5
5
3
3
6
2
2
3
2
2
1
1
1
1
C
C
B
B
A
A
B
B
B
B
B
8
B
B
B
C
C
B
B
B
B
A
A
B
B
B
A
C
C
C
                                                                                          PEDCo  ENVIRONMENTAL
                                                                                                 CINCINNATI. OHIO  4S246

-------
                                          TABLE  1
                               SUMMARY LIST  OF FGD  SYSTEMS
  FGO STATUS REPORT 06/77

  X.O. NUMBER AND COMPANY NAME
        UNIT NAME
       LOCATION
START UP DATE   STATUS
       REG
       CLASS
  106 TEXAS POWER « LIGHT CO.
  107 TEXAS POWER AND LIGHT CO.
  106 TEXAS POWER AND LIGHT CO.
  109 TEXAS UTILITIES
  110 TEXAS UTILITIES CO.
  Ill TEXAS UTILITIES CO.
  112 TEXAS UTILITIES CO.
  113 TEXAS UTILITIES CO.
  11* TEXAS UTILITIES CO.
  115 UNITED POWER ASSOCIATION
  116 UNITED POWER ASSOCIATION
  117 UTAH POWER * LIGHT CO.
  116 UTAH POWER ft LIGHT CO.
  119 WISCONSIN POWER I LIGHT  CO.
     SANOOw NO.*
     TWIN OAKS NO.  1
     TWIN OAKS NO.  2
     FOREST GROVE NO.  1
     MARTIN LAKE NO. 1
     MARTIN LAKE NO. 2
     MARTIN LAKE NO. 3
     MARTIN LAKE NO. H
     MONTICELLO NO.3
     COAL CREEK NO. 1
     COAL CREEK NO. 2
     EMERY NO.l
     HUNTINGTON NO.l
     COLUMBIA NO. 2
ROCKDALE  TEXAS
ROBERTSON COUNTY  TEXAS
ROBERTSON COUNTY  TEXAS
ATHENS  TEXAS
TATUM TEXAS
TATUM TEXAS
TATUM  TEXAS
TATUM  TEXAS
MT. PLEASANT TEXAS
UNDERWOOD NORTH DAKOTA
UNDERWOOD NORTH DAKOTA
EMLRY COUNTY  UTAH
PRICE UTAH
PORTAGE  WISCONSIN
       7-80
       8-83
       9-6*
       0-81
      10-77
       2-78
      12-78
      11-62
       2-78
      11-76
      11-79
       6-76
      12-77
       1-60
5
6
6
6
2
2
3
3
2
3
3
2
2
It  OPERATIONAL UNITS
2.  UNITS UNDER CONSTRUCTION
3.  PLANNED - CONTRACT AWARDED
*.  PLANNED - LETTER OF INTENT SIGNED
5.  PLANNED - REQUESTING/EVALUATING BIDS
6.  CONSIDERING ONLY FGD SYSTEMS
A.  BOILER CONSTRUCTED SUBJECT TO FEDERAL NSPS
B.  BOILER SUBJECT TO STATE STANDARD THAT IS MORE STRINGENT THAN THE FEDERAL NSPS
C.  BOILER SUBJECT To STATE STANDARD THAT IS EQUAL TO OR LESS STRINGENT THAN NSPS
Ot  OTHER
E.  REGULATORY CLASS UNKNOWN

                                                               8
                                                                                          PEDCo  ENVIRONMENTAL
                                                                                                 CINCINNATI. OHIO 45246

-------
      TABLE  2

STATUS OF FGD SYSTEMS
                              PEDCo  ENVIRONMENTAL
                                    CINCINNATI. OHIO

-------
 COMPANY
           TABLE 2
STATUS OF FSD SYSTEMS DURING  06/77
 POWER STATION
                       CURRENT MONTH
1.0. NUMBER    1
ALABAMA ELECTRIC COOP
TOHBIGBEE NO. 2
  225  MW - NEW
COAL   0.6- 1.5 PERCENT SULFUR
PEABOOY ENGINEERING
LIMESTONE SCRUBBING
STARTUP   6/78
    PEABOOY ENGINEERING HAS BEEN AWARDED THE CONTRACT FOR THE INSTALLATION
    OF A LIMESTONE SCRUBBING SYSTEM ON THIS UNIT. A HIGH-EFFICIENCY ESP WILL
    BE INSTALLED UPSTREAM OF THE SCRUBBING SYSTEM TO PROVIDE PRIMARY
    PARTICULATE CONTROL. THE FGO SYSTEM CONTAINS TWO SCRUBBING TRAINS,
    TREATING APPROXIMATELY ?0 PERCENT OF THE FLUE GAS FOR REMOVAL OF SULFUR
    DIOXIDE. STACK GAS REHEAT WILL NOT BE REQUIRED. DURING THE REPORT PERIOD.
    THE UTILITY REPORTED THAT THE TWO SCRUBBER lOWERS, BREECHING, AND ANCIL-
    LARY EOUIPMENT ARE NOW BEING ERECTED AT THE PLANT SITE.
I.D. NUMBER    2
ALABAMA ELECTRIC COOP
TOMBIGBEE NO. 3
  225  MW - NEW
COAL   0.6- 1.5 PERCENT SULFUR
PEABODY ENGINEERING
LIMESTONE SCRUBBING
STARTUP   6/79
    PEABOOY ENGINEERING HAS BEEN AWARDED THE CONTRACT FOR THE INSTALLATION
    OF A LIMESTONE SCRUBBING SYSTEM ON THIS UNIT. A HIGH-EFFICIENCY ESP WILL
    BE INSTALLED UPSTREAM OF THE SCRUBBING SYSTEM TO PROVIDE PRIMARY
    PARTICULATE CONTROL. THE FGO SYSTEM CONTAINS TWO SCRUBBING TRAINS,
    TREATING APPROXIMATELY 70 PERCENT OF THE FLUE GAS FOR REMOVAL OF SULFUR
    DIOXIDE. STACK GAS REHEAT WILL NOT BE REQUIRED. UNIT NO. 3 TURBINE AND
    BOILER ARE CURRENTLY UNDER CONSTRUCTION. NO WORK ON THE SCRUBBER PLANT
    HAS COMMENCED AS OF THIS REPORT PERIOD.
1.0. NUMBER    3
ALLEGHENY POWER SYSTEM
PLEASANTS NO. 1
  625  MW - NEW
COAL H.5 PERCENT SULFUR (MAX)
BABCOCK AND WILCOX
LIME SCRUBBING
STARTUP   3/79
    THE UTILITY REPORTS THAT FOUNDATION WORK IS NEARLY COMPLETE. EQUIPMENT IS
    BEING DELIVERED TO THE PLANT SITE. THE COMMENCEMENT OF FULL-SCALE CON.
    STRUCTION IS IMMINENT. A HIGH-EFFICIENCY ESP AND FOUR SPRAY TOWERS WILL
    BE INSTALLED WITH DESIGN EFFICIENCIES OF 99.5 AND 90 PERCENT RESPEC-
    TIVELY. PILOT STUDIES INDICATE THAT MG ION CONCENTRATION SUPERSEDES ALL
    OTHER EFFICIENCY EFFECTS, AND THE UTILITY MAY SUPPLEMENT DRAVO THIOSORBIC
    WITH DOLOMITE IF NECESSARY.  THE UTILITY ALSO REPORTS THAT PLASlTE W005 IS
    BEING CONSIDERED FOR USE AS  STACK LINING DUE TO VINYL CONTENT.
1.0. NUMBER    <»
ALLEGHENY POWER SYSTEM
PLEASANTS NO. 2
  625  MW - NEW
COAL H.5 PERCENT SULFUR (MAX)
BABCOCK AND WILCOX
LIME SCRUBBING
STARTUP   3/80
    THE THREE PRINCIPAL OPERATING UTILITY COMPANIES OF THE ALLEGHENY POWER
    SYSTEM ARE INSTALLING AN EMISSION CONTROL SYSTEM FOR THIS NEW COAL-FIRED
    UNIT WHICH INCLUDES A HIGH EFFICIENCY ESP UPSTREAM OF FOUR SPRAY TOWERS
    FOR THE CONTROL OF PARTICULATES AND SULFUR DIOXIDE. DESIGN REMOVAL
    EFFICIENCIES FOR THIS EMISSION CONTROL SySTEM ARE 99.5 AND 90 PERCENT,
    RESPECTIVELY. THE ORAVO CO. IS SUPPLYING THIOSORBIC LIME. THE CONSULTING
    ENGINEERING FIRM IS UNITED ENGINEERS AND CONSTRUCTORS. CURRENTLY* FOUNDA-
    TION WORK ON THE SCRUBBER PLANT IS NOW IN PROGRESS.
I.D. NUMBER    5
ARIZONA ELECTRIC POWER COOP
APACHE NO 2
  *0ff '"MW - NEW
COAL  0.5- 0.8 PERCENT SULFUR
RESEARCH COTTRELL
LIMESTONE SCRUBBING
STARTUP   6/78
    SIMULTANEOUS CONSTRUCTION ON BOTH UNITS NO.  2 AND 3 FGD SYSTEMS IS CON-
    TINUING. THE STRUCTURAL STEELWORK FOR THE HOT-SIDE UOP ESP»S IS IN. EREC-
    TION OF THE SCRUBBER-ABSORBER TOWERS IS NEARLY COMPLETE. BOILER CONSTRUC-
    TION HAS NOT BEGUN.  THERE ARE CURRENTLY 2 PONoS WITH A TOTAL OF 20-YRS
    CAPACITY FOR THE DISPOSAL OF THE UNFIXATED SLUDGE. 2 ADDITIONAL PONDS ARE
    PLANNED PROVIDING AN ADDITIONAL 20 YRS OF DISPOSAL CAPABILITY.  THERE WILL
    BE NO REHEAT AND A ZEOLITE LINER IS PLANNED  FOR THE WET STACK*  WHICH WILL
    CONSIST OF A COMMON OUTER SHELL AND A SEPARATE FLUE FOR EACH UNIT.
                                                                                           PEDCo  ENVIRONMENTAL
                                                                                                  CINCINNATI. OHIO 45246

-------
 COMPANY
           TABLE 2
STATUS OF FGU SYSTEMS DURING
06/77
 POWER STATION
                       CURRENT MONTH
1.0. NUMBER    6
ARIZONA ELECTRIC POWER COOP
APACHE NO 3
  200  MW - NEW
COAL   0.5- 0.8 PERCENT SULFUR
RESEARCH COTTRELL
LIMESTONE SCRUBBING
STARTUP   4/79
    SIMULTANEOUS CONSTRUCTION ON BOTH UNITS NO. 2 AND 3 FGD SYSTEMS IS CON-
    TINUING. THE STRUCTURAL STEELWORK FOR TH£ HOT-SIDE UOP tSP'S IS IN. EREC-
    TION OF THE SCRUBBER-ABSORBER TOWERS IS NEARLY COMPLETE. BOILER CONSTRUC-
    TION HAS NOT BEGUN. THERE ARE CURRENTLY 2 PONDS WITH A TOTAL OF 20-YRS
    CAPACITY FOR THE DISPOSAL OF THE UNFIXATEO SLUDGE. 2 ADDITIONAL PONDS ARE
    PLANNED PROVIDING AN ADDITIONAL 20 YRS OF DISPOSAL CAPABILITY. THERE WILL
    BE NO REHEAT AND A ZEOLITE LINER IS PLANNED FOR THE WET STACK. WHICH WILL
    CONSIST OF A COMMON OUTER SHELL AND A SEPARATE FLUE FOR EACH UNIT.
I.D. NUMBER    7
ARIZONA PUBLIC SERVICE
CHOLLA NO 1
  115  MW - RETROFIT
COAL   0.44-1 PERCENT SULFUR
RESEARCH COTTRELL
LIMESTONE SCRUBBING
STARTUP  10/73
    THE BOILER OPERATED 91.6R OF THE TIME IN THE PERIOD INCLUDING MARCH.
    APRIL. « MAY. AVERAGE OPERABILITIES OF THE A-SIOE AND B-SIUE SCRUBBERS
    WEKE 69.4 AND 96.6 PERCENT« RESPECTIVELY. AVERAGE RELIABILITIES OF THE
    TWO SCRUBBERS FOR THE SAME PERIOD WERE 66.4 AND 93.5 PERCENT, RESPEC-
    TIVELY. OUTAGES WERE REQUIRED FOR MID-YEAR CLEANING AND SOME MINOR REPAIR
    WORK. RESEARCH-COTTRELL PERSONNEL ARE CURRENTLY CONDUCTING TESTS AT THIS
    PLANT TO OBSERVE THE EFFECTS OF FORCED SULFITE-TO-SULFATE OXIDATION
    ON THE SCRUBBER PROCESS.
I.D. NUMBER    8
ARIZONA PUBLIC SERVICE
CHOLLA NO 2
  250  MW - NEW
COAL   0.44-1 PERCENT SULFUR
RESEARCH COTTRELL
LIMESTONE SCRUBBING
STARTUP   6/78
    THE CONTRACT FOR THIS WET LIMESTONE SCRUBBING SYSTEM HAS BEEN AWARDED
    BY THE UTILITY TO RESEARCH-COTTRELL. THIS SYSTEM IS A LARGER-SCALE
    APPLICATION OF THE CHOLLA NO.l DESIGN. ALL DESIGN AND ENGINEERING WORK
    HAS BEEN COMPLETED.  THE TURBINE, BOILER AND SCRUBBER ARE UNDER
    CONSTRUCTION.  THE UNIT COMMERICAL START-UP DATE IS SCHEDULED FOR JUNE
    I97a.  THE SCRUBBER PLANT CONSISTS OF FOUR PARALLEL FLOOOED-DISC
    SCRUBBER AND PACKED TOWER ABSORBER TRAINS.  THREE ARE REQUIRED FOR
    FULL LOAD CAPACITY.
I.D. NUMBER    9
ARIZONA PUBLIC SERVICE
CHOLLA NO. *
  350  MW - RETROFIT
COAL  0.44-1 PERCENT SULFUR
NOT DETERMINED
LIMESTONE SCRUBBING
STARTUP   6/80
    UNIT NO. 4 IS CURRENTLY UNDER CONSTRUCTION. APS IS IN THE PRELIMINARY
    DESIGN STAGE FOR INCLUSION OF A WET SCRUBBER PLANT FOR SOg CONTROL.
    THL STATE REGULATORY AGENCY HAS NOT YET DECIDED THE EMISSIONS REGULATIONS
    WHICH WILL APPLY TO THE PLANT. THE C-E BOILER WILL FIRE THE SAME COAL
    AS CHOLLA NO. 1, WITH SULFUR CONTENT OF 0.44-1.0 PERCENT. THE A-C FIRM
    IS EBASCO. COMMERCIAL START-UP IS SLATED FOR 06/80.
I.D. NUMBER   10
ARIZONA PUBLIC SERVICE
FOUR CORNERS NO. 4
  755  MW - RETROFIT
COAL 0.7 PERCENT SULFUR
NOT SELECTED
NOT SELECTED
STARTUP   O/ 0
    THE UTILITY IS CURRENTLY EVALUATING THE DATA AND INFORMATION
    ACCUMULATED DURING THE HORIZONTAL PROTOTYPE SCRUBBING PROGRAM
    IN ORDER TO ASCERTAIN VARIOUS POSSIBLE STRATEGIES TO CONTROL
    THE EMISSIONS FROM THIS COAL-FIRED 755-MW UNIT. A DECISION
    HAS NOT YET BEEN FINALIZED.
                                                                12
                                                                                           PEDCo  ENVIRONMENTAL
                                                                                                  CINCINNATI. OHIO 45246

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 COMPANY

 POWER STATION
           TABLE 2
STATUS OF FGD SYSTEMS DURING
06/77
                       CURRENT MONTH
I.D. NUMBER   11
ARIZONA PUBLIC SERVICE
FOUR CORNERS NO. SB
  755  MW - RETROFIT
COAL 0.7 PERCENT SULFUR
NOT SELECTED
NOT SELECTED
STARTUP   O/ 0
    THE UTILITY IS CURRENTLY EVALUATING THE DATA AND INFORMATION
    ACCUMULATED DURING THE HORIZONTAL PROTOTYPE SCRUBBING PROGRAM
    IN ORDER TO ASCERTAIN VARIOUS POSSIBLE STRATEGICS TO CONTROL
    THE EMISSIONS FROM THIS COAL-FIflED 755-MW UNIT.  A DECISION
    HAS NOT YET BEEN FINALIZED.
    FOR THIS UNIT HAS NOT YET BEEN FINALIZED.
I.D. NUMBER   12
BASIN ELECTRIC POWER COOP
ANTELOPE VALLEY NO. 1
  ISO  Mw • NEW
LIGNITE 1.0 PERCENT SULFUR
NOT SELECTED
LIME/ALKALINE FLYASH SCRUBBING
STARTUP   0/81
    THE UTILITY IS CURRENTLY PLANNING TO INSTALL A WET SCRUBBING SYSTEM TO
    CONTROL S02 EMISSIONS FROM THIS LIGNITE-FIRED BOILER. THE ABSORBENT
    WILL BE EITHER LIME ANo/OR ALKALINE FLYASH.  THIS NEW FACILITY IS
    LOCATED IN THE MERCER COUNTY AREA NEAR BEULAH, NORTH DAKOTA AND IS
    KNOWN AS THE ANTELOPE VALLEY STATION. BOTH UNITS 1 AND 2 WILL BE REQUIRED
    TO COMPLY WITH AIR EMISSION STANDARDS VIA BEST AVAILABLE TECHNOLOGY.
    START-UP IS SCHEDULED FOR 1961.
1.0. NUMBER   13
BASIN ELECTRIC POWER COOP
ANTELOPE VALLEY NO. 2
  HSO  MW - NEW
LIGNITE 1.0 PERCENT SULFUR
NOT SELECTED
NOT SELECTED
STARTUP   0/63
    THE UTILITY IS CURRENTLY INVESTIGATING VARIOUS FGD PROCESSES FOR THIS
    SECOND LIGNITE-FIRED UNIT SCHEDULED AT THIS NEW STATION LOCATED IN MERCER
    COUNTYiNEAR BEULAH,NOHTH DAKOTA.  THIS NEW FACILITY WILL BE KNOWN AS
    THE ANTELOPE VALLEY  STATION AND WILL BE REOUIR£D TO COMPLY WITH AIR
    EMISSION STANDARDS VIA THE BEST AVAILABLE TECHNOLOGY.  START-UP IS NOW
    SCHEDULED FOR 1983.
I.D. NUMBER   m
BASIN ELECTRIC POWER COOP
LARAMIE RIVER NO. 1
  S50  MW - NEW
COAL  0.6 PERCENT SULFUR
RESEARCH COTTRELL
LIMESTONE SCRUBBING
STARTUP   "»/80
    RESEARCH-COTTRELL IS CURRENTLY  FABRICATING THE DUAL-LOOP LIMESTONE WET
    SCRUBBERS.  NO ON.SITE CONSTRUCTION HAS YET BEGUN.  NO SLUDGE DISPOSAL CON.
    TRACT HAS AS YET BEEN AWARDED.  BUT THE DISPOSAL STRATEGY WILL BE ONE
    WHICH OEWATERS THE SLUDGE TO 63 PERCENT SOLIDS PRIOR TO DISPOSAL.
    THE LARAMIE RlyER STATION WILL  UTILIZE A SUB-BITUMINOUS COAL WITH A
    HEATING VALUE OF 6100 BTU/LB AND SULFUR AND ASH CONTENTS OF 0.6 PERCENT
    AND 7.0 PERCENTt RESPECTIVELY.  THE CAPITAL COST FOR THL FGD SYSTEM IS
    ESTIMATED AT 60 MILLION DOLLARS.
I.D. NUMBER   15
BASIN ELECTRIC POWER COOP
LARAMIE RIVER NO. 2
  550  MW - NEW
COAL  0.6 PERCENT SULFUR
RESEARCH COTTRELL
LIMESTONE SCRUBBING
STARTUP  10/60
    RESEARCH-COTTRELL IS CURRENTLY FABRICATING THE DUAL-LOOP LIMESTONE WET
    SCKUBBERS.  NO ON-SlTE CONSTRUCTION HAS YET BEGUN.  NO SLUDGE DISPOSAL CON'
    TRACT HAS AS YET BEEN AWARDED, BUT THE DISPOSAL STRATEGY WILL BE ONE
    WHICH DEWATERS THE SLUDGE TO 63 PERCENT SOLIDS PRIOR TO DISPOSAL.
    THE LARAMIE RIVER STATION WILL UTILIZE A SUB-BITUMINOUS COAL WITH A
    HEATING VALUE OF 6100 BTU/LB AND SULFUR AND ASH CONTENTS OF 0.6 PERCENT
    AND 7.0 PERCENT, RESPECTIVELY. THE CAPITAL COST FOR THE FGD SYSTEM Is
    ESTIMATED AT 60 MILLION DOLLARS.
                                                                13
                                                                                          PEDCo  ENVIRONMENTAL
                                                                                                 CINCINNATI. OHIO 45246

-------
 COMPANY

 POWER STATION
           TABLE 2
STATUS OF F6D SYSTEMS DURING  06/77

                       CURRENT MONTH
1.0. NUMBER   16
BASIN ELECTRIC POWER COOP
LARAMIE RIVER NO. 3
  950  MU • NEW
COAL  0.6 PERCENT SULFUR
NOT SELECTED
NOT SELECTED
STARTUP   6/63
    THE. UTILITY IS STILL CONSIDERING VARIOUS F6D PROCESSES. LARANlE RIVER
    STATION WILL FIRE SUB-BITUMINOUS COAL WITH THE FOLLOWING CHARACTERIS-
    TICS* 6100 BTU/LBi 0.6 PERCENT SULFUR AND 7.0 PERCENT ASH.
1.0. NUMBER   17
BI6 RIVERS ELECTRIC COOP CORP.
REID NO. 2
  250  MW » NEW
COAL 3.5-<».0 PERCENT SULFUR
AMERICAN AIR FILTER
LIME SCRUBBING
STARTUP  12/79
    THE EMISSION CONTROL SYSTEM FOR THIS NEW COAL-FIRED UNIT IS BEING SUPP-
    LIED BY AMERICAN AIR FILTER. THE SYSTEM WILL CONSIST OF A COLO.SIDE ESP
    AND TWO SPRAY TOWERS CONTROLLING PARTICIPATE AND SOg TO 99.6 PERCENT AND
    90 PERCENT. RESPECTIVLEV, THE saw BOILER WILL FIRE HIGH SULFUR ta.s TO
    H.5 PERCENT! WESTERN KENTUCKY COAL. FGD SYSTEM FOUNDATIONS HAVE BEEN
    LAID, BUT NO ON.SITE ASSEMBLY HAS COMMENCED. A SLUDGE FIXATION STRATEGY
    is PLANNED, BUT NO CONTRACT HAS BEEN AWARDED. THE FGD SYSTEM WILL BE
    FOLLOWED BY STEAM-TUBE REHEAT BUNDLE.
I.D. NUMBER   16
BRAZOS ELECTRIC POWER COOP
ATACOSA MCMULLEN NO. 1
  HOO  MW - NEW
LIGNITE 1.67 PERCENT SULFUR
BABCOCK ft WILCOX
LIMESTONE SCRUBBING
STARTUP  12/79
    THE EMISSION CONTROL EQUIPMENT FOR THE COAL-FIRED RADIANT BOILER WILL
    CONSIST OF AN E.S.P. UPSTREAM OF FOUR LIMESTONE SCRUBBING MODULES.
    THE SCRUBBER FLUE GAS CAPACITY IS NOMINALLY DESIGNED AT 1.579 MILLION
    ACFM (302 F).  DESIGN S02 REMOVAL EFFICIENCY IS 66 PERCENT FOR t«»00 PPM
    S02 INLET. THE BOILER WILL BE FIRED WITH 436 TON/HR OF LIGNITE,  THE
    SCRUBBING WASTES WILL BE DISPOSED OF IN AN OFF.SITE MINEFILL.  FGD SYSTEM
    CONSTRUCTION IS CURRENTLY SCHEDULED TO BEGIN IN EARLY 1976.  BOILER
    START-UP is SCHEDULED FOR 01/79 WITH FGD START-UP SET FOR 12/79.
I.D. NUMBER   19
CENTRAL ILLINOIS LIGHT CO.
DUCK CREEK NO. 1
  «»00  MW - NEW
COAL 2.5 - 3.0 PERCENT SULFUR
RILEY STOKER/ENVIRONEERING
LIMESTONE SCRUBBING
STARTUP   8/78
    A CONTRACT HAS BEEN AWARDED BY THE UTILITY TO THE RILEY STOKER CORP. FOR
    THE DESIGN* FABRICATION AND INSTALLATION OF FOUR VENTRI-SORBER MODULES
    TO TREAT THE FLUE GAS FROM THIS COAL-FIRED STEAM BOILER.  THE FIRST
    LIMESTONE SLURRY SCRUBBER MODULE WAS PLACED IN SERVICE ON SEPTEMBER 9.
    1976, AND OPERATED INTERMITTENTLY UNTIL APRIL 1, 1977.  A HIGH EFFICIENCY
     ESP IS INSTALLED UPSTREAM OF FOUR VENTRI-SORBER SCRUBBER MODULES FOR
    PARTICULATE CONTROL.  DESIGN PARTICIPATE AND SULFUR DIOXIDE REMOVAL
    EFFICIENCIES ARE 99.8 AND 75 PERCENT,RESPECTIVELY.
I.D. NUMBER   20
CENTRAL ILLINOIS LIGHT CO.
DUCK CRELK NO.2
  HOO  MW - NEW
COAL 2.5-3.0 PERCENT SULFUR
NOT SELECTED
LIMESTONE SCRUBBING
STARTUP   1/62
    THE PROPOSED LIMESTONE SCRUBBING SYSTEM FOR THIS NEW COAL-FIRED
    UNIT is SCHEDULED TO COMMENCE OPERATIONS IN JANUARY 1952. THE
    UTILITY HAS NOT YET SELECTED A SYSTEM SUPPLIER, A DECISION CONCERNING
    THE STATUS OF THE BOILER AND CONTROL STRATEGY WILL BE ANNOUNCED
    DURING THE LATTER PART OF 1977,
                                                                                           PEDCo  ENVIRONMENTAL
                                                                                                  CINCINNATI. OHIO -45246

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 COMPANY

 POWER STATION
           TABLE 2
STATUS OF FGD SYSTEMS DURING
06/77
                       CURRENT MONTH
1.0* NUMBER   21
CENTRAL ILLINOIS PUBLIC SERV
NEWTON NO.l
  579  MM - NEW
COAL 2.6-3*2 PERCENT SULFUR
BUELL/ENVIROTECH
DOUBLE ALKALI SCRUBBING
STARTUP  11/79
    A CONTRACT HAS BEEN AWARDED BY CIPSCO TO BUELL/ENVIROTECH FOR THE
    INSTALLATION OF AN EMISSION CONTHOL SYSTEM ON UNIT N0.lt A COAL-FIRED
    575-MW POWER BOILER LOCATED IN NEwTON.ILLINOIS. THE KEY COMPONENTS OF THE
    EMISSION CONTROL SYSTEM INCLUDE* A HIGH-EFFICIENCY ESP, FOUR PRECOOLERS,
    FOUR POLVSPHERE ABSORBERS, THREE THICKENERS. TWO EXPERIMENTAL REHEAT S
    SYSTEMS. AND THREE HORIZONTAL EXTRACTION FILTERS FOR SLUDGE DEMATERING. E
    AT PRESENT, 15 PERCENT OF THE CONSTRUCTION WORK AT THE PLANT HAS BEEN
    COMPLETED. THE FgO SYSTEM WILL HAVE CEILCOTE-LINEO ABSORBER MODULES.
I.0. NUMBER   22
CINCINNATI GAS ft ELECTRIC CO.
EAST BEND NO 2
  600  MW . NEW
COAL
NOT SELECTED
NOT SELECTED
STARTUP   1/81
    BIO REQUEST AND EVALUATION IS SCHEDULED TO COMMENCE SHORTLY.
    CONSTRUCTION AND OPERATING PERMITS ARE BElNtt PROCURED. A COAL
    SOURCE AND SUPPLY HAS NOT BEEN FINALIZED. COMMERCIAL
    START-UP DATE HAS BEEN DELAYED ONE YEAR TO JANUARY 1981.
    THE A-E DESIGN FIRM IS SARGENT AND LUNDY.
I.D. NUMBER   23
COLORADO UT£ ELECTRIC ASSN.
CRAIG NO. 1
  •ISO  MW - NEW
COAL O.H5 PERCENT SULFUR
PEABODY ENGINEERING
LIMESTONE SCRUBBING
STARTUP   3/79
    PEABODY ENGINEERED SYSTEMS HAS BEEN AWARDED A CONTRACT IN EXCESS OF
    S60 MILLION TO DESIGN AND SUPPLY A LIMESTONE SLURRY SPRAY TOWER
    SCRUBBING SYSTEM FOR SULFUR DIOXIDE REMOVAL FROM LOW-SULFUR COAL-FIRED
    BOILER FLUE GAS.  PARTICULATE CONTROL WILL BE PROVIDED BY HOT-SIDE
    ESP'S UPSTREAM OF THE SCRUBBER PLANT.
    REQUIRED PARTICULATE AND SULFUR DIOXIDE REMOVAL EFFICIENCIES ARE 99.8
    AND 85 PERCENT, RESPECTIVELY. FGD START-UP IS SCHEDULED FOR SPRING 1979.
I.D. NUMBER   21
COLORADO UTE ELECTRIC ASSN.
CRAIG NO. 2
  ISO  MW - NEW
COAL 0.<»5 PERCENT SULFUR
PEABODY ENGINEERING
LIMESTONE SCRUBBING
STARTUP   3/79
    PEABODY ENGINEERED SYSTEMS HAS BEEN AWARDED A CONTRACT IN EXCESS OF
    $60 MILLION TO DESIGN AND SUPPLY A LIMESTONE SLURRY SPRAY TOWER
    SCRUBBING SYSTEM FOR SULFUR DIOXIDE REMOVAL FROM LOW-SULFUR COAL-FIRED
    BOILER FLUE GAS.  PARTICULATE CONTROL WILL BE PROVIDED BY HOT-SIDE
    ESP'S UPSTREAM.OF THE SCRUBBER PLANT.
    REQUIRED PARTICULATE AND SULFUR DIOXIDE REMOVAL EFFICIENCIES ARE 99.8
    AND 85 PERCENT. RESPECTIVELY. FGD START-UP IS SCHEDULED FOR SPRING 1979.
I.D. NUMBER   25
COLUMBUS ft SOUTHERN OHIO ELEC.
CONESVILLE NO 5
  HOO  MW - NEW
COAL  ».5 - *.9 PERCENT SULFUR
UNIVERSAL OIL PRODUCTS
LIME SCRUBBING
STARTUP   2/77
    REFER TO THE BACKGROUND INFORMATION SECTION IN TABLE 5 OF THIS REPORT.
    THE BOILER AND ESP WERE COMPLETED AND PLACED IN SERVICE IN SEPT.  1976.
    THE B-SIDE MODULE BECAME AVAILABLE FOR SERVICE IN JANUARY 1977.
    COMMERCIAL OPERATIONS WERE ACHIEVED ON FEBRUARY 13.  1977. THE EMISSION
    CONTROL SYSTEM FOR THIS UNIT CONSISTS OF A COLD.SIDE ESP FOLLOWED BY
    TWO TCA LIME SCRUBBING MODULES SUPPLIED BY UOP. DRAVO IS SUPPLYING THE
    THIOSORBIC LIME SCRUBBING REAGENT. IUCS IS SUPPLYING THEIR POZ-0-TEC
    SLUDGE STABILIZATION FACILITY. B-SIDE STARTUP IS SCHEDULED FOR JAN. 1978.
                                                                15
                                                                                           PEDCo  ENVIRONMENTAL
                                                                                                  CINCINNATI. OHIO 45246

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 COMPANY

 POWER STATION

1.0. NUMBER   26
COLUMBUS ft SOUTHERN OHIO ELCCt
CONESVILLE NO 6
  HOO  AW - NEW
COAL  *.S - «».9 PERCENT SULFUR
UNIVERSAL OIL PRODUCTS
LIME SCRUBBING
STARTUP   1/78
            TABLE  2
 STATUS OF  F60 SYSTEMS  DURING   06/77

                        CURRENT MONTH

	THE~UTIL1TY~SIGNEO~UONG-TERM CONTRACTS WITH ORAVO FOR THE PURCHASE OF
    THIOSORBIC LIME  AND WITH  IUCS FOR  THE PURCHASE OF SLUDGE FIXATIVES.  CON-
    STRUCTION OF  THIS  UNIT  COMMENCED IN 1977  AND IS SCHEDULED TO BE
    COMPLETED BY  JANUARY 1976. SIMILAR TO CONESVILLE NO.5,  THIS MINE MOUTH
    PLANT  WILL BURN  COAL WITH 17 PERCENT ASH  CONTENT AND  <».9 TO i».9 PERCENT
    SULFUR CONTENT.  AN ELECTROSTATIC PRLClPITATOR MILL BE INSTALLED UPSTREAM
    THE FGD SYSTEM.  THE FGD SYSTEM WILL INCLUDE TWO TCA MODULES FOR THE RE-
    MOVAL  OF S02.  THE  A-E DESIGN FIRM  IS BLACK AND VEATCH.
I.D. NUMBER   27
COLUMBUS 1 SOUTHERN OHIO ELEC.
POSTON NO. 5
  975  MW • NEW
COAL 2.9 PERCENT SULFUR
NOT SELECTED
NOT SELECTED
STARTUP   0/81
     THIS UNIT  WILL BURN HIGH SULFUR OHIO COAL I APPROXIMATELY 2.5 PERCENT
     SULFUR  CONTENT).  THE DESIGN OF THE EMISSION CONTROL STRATEGY HAS
     NOT  YET BEEN  FINALIZED.
I.D. NUMBER   28
COLUMBUS * SOUTHERN OHIO ELEC.
POSTON NO. 6
  975  MW - NEW
COAL 2.5 PERCENT SULFUR
NOT SELECTED
NOT SELECTED
STARTUP   0/83
     THIS UNIT  WILL BURN HIGH SULFUR COAL (APPROXIMATELY 2.5 PERCENT
     SULFUR  CONTENT).  THE DESIGN OF THE EMISSION CONTROL STRATEGY
     FOK  THIS UNIT  HAS NOT YET BEEN FINALIZED.
1.0. NUMBER   29
COMMONWEALTH EDISON
POWERTON NO. 51
  t25  MM - RETROFIT
COAL 3.6 PERCENT SULFUR
UNIVERSAL OIL PRODUCTS
LIMESTONE SCRUBBING
STARTUP  12/79
     UOP WAS AWARDED THE CONTRACT FOR THE INSTALLATION OF A WET LIMESTONE
     SCRUBBING SYSTEM THAT HILL BE BACKFITTED ONTO BOILER NO.51. ONE OF TWO
     IDENTICAL BOILERS SUPPLYING STEAM TO AN 850-MW TURBINE-GENERATOR*  THE
     FGO SYSTEM IS DESIGNED TO TREAT FLUE GAS RESULTING FROM THE COMBUSTION
     OF HIGH SULFUR COAL (3.6 PERCENT SULFUR* 8.3 PERCENT ASH* 17.3 PERCENT
     MOISTURE* 10.500 BTU/LB.) AND MEET S02 EMISSION STANDARDS OF 1.8 Lfl.
     S02/MM BTU.  CURRENTLY. EXCAVATION. BACKFILL. AND STRUCTURAL STEEL
     ERECTION IS  IN PROGRESS.
I.D* NUMBER   30
COMMONWEALTH EDISON
WILL COUNTY NO 1
  167  MW - RETROFIT
COAL «.o PERCENT SULFUR
BABCOCK I WILCOX
LIMESTONE SCRUBBING
STARTUP   2/72
     REFER TO THE BACKGROUND INFORMATION SECTION IN TABLE 5 OF THIS REPORT.
     THIS FULL SCALE DEMONSTRATION SCRUBBING SYSTEM HAS BEEN IN SERVICE SINCE
     FEBRUARY 1972.  THE FGD SYSTEM INCLUDES TWO SCRUBBING TRAINS FOR THE
     CONTROL OF PARTICULATES AND SULFUR DIOXIDE. MODULE AVAILABILITY*
     OPLRABILITY* RELIABILITY*  AND UTILIZATION INDEX VALUES FOR THE REPORT
     PERIOD ARE PROVIDED IN TABLE 5.  A SLUDGE STUDY. CONDUCTED BY UOP*  AND A
     MAGNESIUM INNOCULATION AND FORCED OXIDATION STUDY, CONDUCTED BY THE
     UTILITY* WERE COMPLETED DURING THE REPORT PERIOD.
                                                                16
                                                                                             PEDCo  ENVIRONMENTAL.
                                                                                                   CINCINNATI. OHIO

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 COMPANY
           TABLE 2
STATUS OF FGD SYSTEMS DURING
                              06/77
 POWER STATION
                       CURRENT MONTH
1.0. NUMBER   31
OUQUESNC LIGHT
CLRAMA POWER STATION
  310  MW . RETROFIT
COAL  1.0 - 2.B PERCENT SULFUR
CHEMICO
LIME SCRUBBING
STARTUP  10/75
    REFER TO THE BACKGROUND INFORMATION SECTION IN TABLE 5 OF THIS REPORT.
    OPERATIONS ARE CONTINUING WITH TWO BOILERS COUPLED INTO THL FIVE-MODULE
    SCRUBBING SYSTEM. RUBBER-LINED RECYCLE PUMPS HAVE BEEN REMOVED FROM TEST-
    ING AS THEY WERE UNDERGOING SEVERE ABRASION AND GOUGING. ANOTHER SET OF
    RUBBER-LINED PUMPS MAY BE TESTED. SCRUBBING WASTES ARE CHEMICALLY FIXATED
    BY THE IUCS METHOD AND LANDFILLED. UUOUE.SNE LIGHT IS CONTINUING EFFORTS
    TO OBTAIN ALTERNATE LANDFILL AREAS AS I HE CURRENT ONES ARE BEING FILLED
    FAIRLY RAPIDLY.
1.0. NUMBER   32
OUOUESNE LIGHT
PHILLIPS POWER STATION
  410  MW - RETROFIT
COAL   1.0- 2.6 PERCENT SULFUR
CHEMICO
LIME SCRUBBING
STARTUP   7/73
    REFER TO THE BACKGROUND INFORMATION SECTION IN TABLE 5 OF THIS REPORT.
    THIS SCRUBBING SYSTEM HAS BEEN IN SERVICE SINCE JULY 1973. FOUR BOILERS
    CUKRENTLY ARC COUPLED INTO THE SCRUBBING SYSTEM. THE OTHER TWO BOILERS
    ARE DOWN FOR MAINTENANCE. THE SCRUBBER SYSTEM WAS SHUT DOWN FOR ABOUT •*
    DAYS IN MAY DUE TO LEAKING IN THE WET GAS HEADER THAT CONNECTS THE STACK.
    OVERALL SCRUBBER AVAILABILITY HAS BEEN ABOUT 75 PERCENT OUKING THE RE-
    PORTING PERIOD. DEWATEREO SLUDGE FROM THE IUCS INTERIM PROCESSING PLANT
    IS BEING HAULED TO AN OFF-SITE LANDFILL. THE SLUDGE CONTAINS NO FIXATIVE.
I.D. NUMBER   33
EASTERN KENTUCKY POWER COOP
SPURLOCK GENERATING PLANT NO,2
  SOO  MW - NEW
COAL
NOT SELECTED
NOT SELECTED
STARTUP   3/80
    THE SPURLOCK GENERATING PLANT IS LOCATED APPROXIMATELY 3 MILES WEST OF
    MAYSVILLE,KENTUCKY, TWO NEW UNITS ARE SCHEDULED FOR THIS STATION. UNIT
    NO.l WILL BEGIN OPERATION IN EARLY JULY* IT DOES NOT HAVE TO MEET NSPS.
    THE CONTRACTED COAL FOR UNIT NO.l WILL MEET S02 COMPLIANCE. UNIT NO.2
    BE CONTROLLED BY A 99.5 PERCENT EFFICIENT ESP. OESULFURIZATlON MAY BE
    RE8UIRED IF THE UTILITY CANNOT SECURE A LTERM ONG-CONTRACT FOR THE
    PURCHASE OF LOW-SULFUR COAL. THE UTILITYSIS NECURING THE SERVICES OF AN
    A-E FIRM IN THE EVENT AN FGD SYSTEM IS REED.R
I.D. NUMBER   3
-------
 COMPANY

 POWER STATION
           TABLE 2
STATUS OF F60 SYSTEMS DURING  06/77

                       CURRENT MONTH
1.0. NUMBER   36
KANSAS CITY POWER ft LIGHT
HAWTHORN NO. 3
  mo  nw • RETROFIT
COAL   0.5-3.5 PERCENT SULFUR
COMBUSTION ENGINEERING
LIME SCRUBBING
STARTUP  11/72
    REFER TO THE BACKGROUND INFORMATION SECTION IN TABLE s OF THIS REPORT.
    THE SCRUBBER PLANT HAS BEEN CONVERTED FROM A LIMESTONE FURNACE INJECTION
    AND TAIL-END SCRUBBING STRATEGY TO A TAIL-END WET LIME SCRUBBING STRATEGY
    LIME-BASED OPERATIONS COMMENCED ON FEBRUARY 7, 1977. COMPLIANCE TESTING
    FOR KANSAS CITY PARTICIPATE STANDARDS INDICATED THE NO.3 UNIT W«S WELL
    WITHIN THE 0.17 POUND REGULATION. THE 2-MODULE SCRUBBER PLANT WAS IN
    SERVICE 006 HOURS IN APRIL (57 PERCENT OPERABILITY) AND 302 HOURS IN MAY
    (58 PERCENT OPERABILITY).
I.D. NUMBER   37
KANSAS CITY POWER t LIGHT
HAWTHORN NO, n
  100  MW - RETROFIT
COAL   0.5-3.5 PERCENT SULFUR
COMBUSTION ENGINEERING
LIME SCRUBBING
STARTUP   6/72
    REFER TO THE BACKGROUND INFORMATION SECTION IN TABLE s OF THIS REPORT.
    THE. SCRUBBER PLANT HAS BEEN CONVtRTEO FROM A LIMESTONE FURNACE INJECTION
    AND TAIL-END SCRUBBING DESIGN TO A TAIL-END WET LIME SCRUBBING SYSTEM.
    OPERATIONS IN THE LIME SCRUBBING MODE COMMENCED ON JANUARY It 1977.
    COMPLIANCE TESTING FOR KANSAS CITY PARTICU|.ATE REGULATIONS INDICATED THE
    UNIT IS MEETING THE 0.17 POUND REGULATION. THL 2-MOOULE SCRUBBER PLANT
    WAS IN SERVICE 311 HOURS IN APRIL («»3 PERCENT OPERABILITY) AND 160 HOURS
    IN MAY (5H PERCENT OPERABILITY).
I.D. NUMBER   36
KANSAS CITY POWER * LIGHT
LA CYGNE NO 1
  620  MW - NEW
COAL S.O PERCENT SULFUR
BABCOCK ft WILCOX
LIMESTONE SCRUBBING
STARTUP   2/73
    REFER TO THE BACKGROUND INFORMATION SECTION IN TABLE s OF THIS REPORT.
    THE. EMISSION CONTROL SYSTEM FOR THIS NEW COAL-FIRED POWER-GENERATING UNIT
    CONSISTS OF EIGHT SCRUBBER MODULES FOR FLY ASH AND S02 REMOVAL. EACH
    MODULE INCLUDES A VENTURI SCRUBBED IN SERIES WITH A 2-STAGE IMPINGEMENT
    PLATE ABSORBER.  THE SCRUBBER PLANT IS AN INTEGRAL PART OF THE POWER-
    GENERATING COMPLEX, ALLOWING NO FLUE GAS BYPASS.  INITIAL OPERATIONS
    COMMENCED IN FEB. 1973. COMMERCIAL SERVICE WAS ATTAINED BY JUNE 1973.
    TOTAL SYSTEM AVAILABILITY FOR THE MONTH OF APRIL WAS 93 PERCENT.
1.0. NUMBER   39
KANSAS POWER ft LIGHT
JEFFERY NO. 1
  660  MW - NEW
COAL 0.30 PERCENT SULFUR
COMBUSTION ENGINEERING
LIMESTONE SCRUBBING
STARTUP   6/76
    THE UTILITY HAS PURCHASED AN AIR QUALITY CONTROL SYSTEM FROM COMBUSTION
    ENGINEERING FOR PARTICIPATE AND S02 REMOVAL. THE SYSTEM WILL CONSIST OF
    A COLO-SIDE ESP, I.D. FANS, BY-PASS CAPABILITY, AND SPRAY TOWERS. AN
    OVERFIRE AIR SYSTEM AT THE TANGENTIAL FIRED PULVERIZED BURNERS WILL CON-
    TROL THE NOX EMISSIONS. THE CLEANED GASES WILL BE VENTED TO A 600 FOOT
    STACK. THE CONSTRUCTION OF THIs NEW INSTALLATION Is PROCEEDING
    ACCORDING TO SCHEDULE. THIS UNIT WILL FIRE 250 TONS/HR OF WYOMING
    COAL WITH A HEAT CONTENT OF 8000 BTU/LBt O.jl SULFUR AND 6* ASH.
1.0. NUMBER   <»0
KANSAS POWER ft LIGHT
JEFFERY NO. 2
  680  MW . NEW
COAL 0.30 PERCENT SULFUR
COMBUSTION ENGINEERING
LIMESTONE SCRUBBING
STARTUP   6/79
    THE UTILITY HAS PURCHASED AN AIR QUALITY CONTROL SYSTEM FROM COMBUSTION
    ENGINEERING FOR PARTICIPATE AND S02 REMOVAL. THE SYSTEM WILL CONSIST OF
    A COLO-SIDE ESP, I.D. FANS,  BYPASS CAPABILITY, AND SPRAY TOwERS. AN
    OVE.RFIRE AIR SYSTEM AT THE TANGENTIAL FIRED PULVERIZED BURNERS WILL CON-
    TROL THE NOX EMISSIONS. THE CLEANED GASES WILL BE VENTED To A 600 FOOT
    STACK. THE CONSTRUCTION OF THIS NEW INSTALLATION IS PROCEEDING
    ACCORDING TO SCHEDULE. THIS UNIT WILL 250 TONS/HR OF WYOMING
    COAL HAVING A HEAT CONTENT OF 8000 BTU/LB, 0.3X SULFUR AND 6X ASH.
                                                                16
                                                                                           PEDCo  ENVIRONMENTAL
                                                                                                  CINCINNATI, OHIO 45248

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 COMPANY
 POWER STATION
           TABLE 2
STATUS OF FGO SYSTEMS DURING
                                                                06/77
                       CURRENT MONTH
I.D. NUMBER   41
KANSAS POWER * LIGHT
LAWRENCE NO 4
  125  MW - RETROFIT
COAL 0.5 PERCENT SULFUR
COMBUSTION ENGINEERING
LIMESTONE SCRUBBING
STARTUP  12/68
    REFER TO BACKGROUND INFORMATION SECTION IN TABLE 5 OF THIS REPORT.
    THE NEW LIMESTUNE FcD SYSTEM COMMENCED OPERATIONS IN EAHLY JANUARY 1977.
    THERE HAVE BEEN NO FORCED SCRUBBER OUTAGES SINCE START-UP.
    CONTINUOUS S02 MONITORS ARE RECORDING S02 REMOVAL EFFICIENCIES
    BETTER THAN 85 PERCENT. PARTICULATE REMOVAL IS REPORTED TO
    BE EXCELLENT.  YIELDING NO VISIBLE PLUME,  MINOR PROBLEMS HAVE
    REVOLVED AROUND MAINTAINING SOLIDS LEVELS. SEVERAL DIFFERENT
    TYPES OF SLURRY PUMPS ARE BEING COMPARED  UNDER OPERATING CONDITIONS,
I.D. NUMBER   42
KANSAS POWER I LIGHT
LAWRENCE NO 5
  400  MW . NEW
COAL 0.5 PERCENT SULFUR
COMBUSTION ENGINEERING
LIMESTONE SCRUBBING
STARTUP   6/76
    REFER TO THE BACKGROUND INFORMATION SECTION IN TABLE 5 OF THIS REPORT.
    THt ORIGINAL LIMESTONE INJECTION AND TAIL-END SCRUBBING SYSTEM IS STILL
    IN SERVICE WHILE A NEW ROD-SCRUBBER AND SPRAY TOwER ABSORBER SYSTEM IS
    BEING ERECTED ALONGSIDE THE EXISTING SYSTEM.  THE NEW SCRUBBER PLANT
    INCLUDES 2 MODULES EACH CAPABLE OF HANDLING APPROXIMATELY 50X OF THE TO-
    TAL BOILER FLUE GAS FLOW.  THE SYSTEM DESIGNER AND SUPPLIER IS COMBUSTION
    ENGINEERING. THE UNIT FIRES APPROXIMATELY 140 TONS/HOUR OF LOW SULFUR
    WYOMING COAL HAVING HEAT AND SULFUR CONTENTS  OF 10,000 BTU/LB AND 0.5X.
I.D. NUMBER   43
KENTUCKY UTILITIES
GREEN RIVER NOS. 1  2  AND
   64  MW - RETROFIT
COAL  3.6 PERCENT SULFUR
AMERICAN AIR FILTER
LIME SCRUBBING
STARTUP   9/75
    REFER TO BACKGROUND INFORMATION SECTION IN TABLE 5 OF THIS REPORT.
    STACK REPAIRS WERE COMPLETED DURING THE REPORT PERIOD* AND BOILER
    SCRUBBER OPERATIONS RESUMED IN APRIL,  THE STACK is NOW LINED WITH
    PRECRETE G-8, A REFRACTORY LINING APPLIED BY AAF. DURING APRIL,  OPERA-
    BILITY AND RELIABILITY INDEX VALUES WERE 98*.  AND THE AVAILABILITY  INDEX
    WAS 40X. DURING MAY,  OPERABILITY AND RELIABILITY INDEX VALUES WERE  98»,
    AND THE AVAILABILITY  INDEX VALUE WAS 99*.
I.D. NUMBER   44
LOUISVILLE GAS & ELECTRIC
CANE RUN NO 4
  176  MW - RETROFIT
COAL 3.5 - 4.0 PERCENT SULFUR
AMERICAN AIR FILTER
LIME SCRUBBING
STARTUP   6/76
    REFER TO THE BACKGROUND INFORMATION SECTION IN TABLE 5 OF THIS REPORT.
    SCRUBBER OPERATIONS WERE TERMINATED APRIL IB FOR  THE IMPLEMATION OF
    SEVERAL MODIFICATIONS TO THE FGD SYSTEM,  A CHEVRON-TYPE MIST ELIMINATOR
    WILL BE INSTALLED,  A NEW SPRAY HEADER  WILL INCREASE L/G,  REHEAT WILL
    BE ADDED AND THE CARBOLINE DUCT LINING WILL BE REPLACED WITH
    PLASTITE 4005 (BY GENERAL COATINGS).   THE MODIFICATIONS ARE  EXPECTED TO
    BE COMPLETE BY JULY 5.
I.D. NUMBER   45
LOUISVILLE GAS * ELECTRIC
CANE RUN NO 5
  183  MW . RETROFIT
COAL 3.5 - 4.0 PERCENT SULFUR
COMBUSTION ENGINEERING
LIME SCRUBBING
STARTUP  12/77
    THE UTILITY HAS SIGNED A CONSENT  AGREEMENT  WITH THE EPA FOR  THE  INSTAL-
    LATION AND OPERATION OF FGO EQUIPMENT  ON  THIS UNIT  BY  DECEMBER  Iil977.
    THE CONTRACT FOR THIS LIME  SCRUBBING SYSTEM HAS BEEN AWARDED TO
    COMBUSTION ENGINEERING. THE SYSTLM  IS  NOW UNDER CONSTRUCTION.  WORK  IS
    IN PROGRESS ON THE  FOUNDATION  AND ERECTION  OF STRUCTURAL STEEL.  CON-
    STRUCTION OF THE FGD SYSTEM WAS DELAYED BECAUSE OF  RE8UIREO  FGD  MODIFI-
    CATIONS ON BOILER 4.  BOILER 5 FGD  WORK wILL BE DELAYED ABOUT  45 DAYS.
                                                                19
                                                                                           PEDCo  ENVIRONMENTAL
                                                                                                 CINCINNATI. OHIO

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 COMPANY

 POWER STATION
           TABLE: 2
STATUS OF FGD SYSTEMS DURING
0&/77
                       CURRENT MONTH
I.D. NUMBER   <*6
LOUISVILLE GAS X ELECTRIC
CANE RUN NO 6
  277  NW - RETROFIT
COAL 3.3 - 4.0 PERCENT SULFUR
ADL/COMiMJSTlON EQUIP ASSOCIATE
DOUBLE A'.KALI SCRUBBTNC
STARTUP   2/79
    THE CONTRACT FOR THIS FULL-SCALE  DEMONSTRATION SCRUBBING SYSTEM HAS BEEN
    AWARDED TO A,0.LITTLE/COMBUSTI ON  EQUIPMENT  ASSOC.  FOR THE INSTALLATION
    OF A DOUBLE ALKALI SCRUBBER,  THE  FEDERAL  EPA  WILL  SUBSIDIZE A MAXIMUM
    SU.5 MM FOR OPERATION. RESEARCH AND  DEVELOPMENT,  A'.'D "F.POHT WRITING FOR
    ,\ ONE-YEA1' PERIOD FOLLOWING  THE FIRST  THR[.[. MONTHS <,F- OPtRfl T I Orj (NOjf.a THl S
    SUBSIDY KILL. NUT BF. APPLIED  F:OR ANT  rr^lTAI. EXPENUI fUSES ) ,  ENGINEERING
    DESIGN WORK IS NOW UNOLRHAy,  START-UP  IS  SCHEDULED "OH FEBRUARY 1.JL979.
I.D. NUMBER   i»7
LOUISVILLE GAS I. ELECTRIC
MILL C"EEK NO 1
  330  H*l - RETROFIT
COAL   3.5- <*.0 PERCENT SULFUR
NOT SELECTED
LIME SCRUBBING
STARTUP   1/82
    A COMPLIANCE SCHEDULE: HAS  BEEN  SUBMITTED TO THE; JEPI--IRSOM COUNTY AIH POL-
    LUTION CONTROL DISTRICT  WITH  1/B2  ESTABLISHED AS I'ME STARTUP 0,',TC. ; OR AN
    FGU SYSTEM,
I.D. NUMBER   H8
LOUISVILLE GAS 4 ELECTRIC
MILL CREEK NO S
  330  HW - RETROFIT
COAL   3.5- "».0 PERCENT SULFUR
NOT SELECTED
LIME SCRUBBING
STARTUP   1/B1
    A COMPLIANCE SCHEDULE HAS  BEEN  SUBMITTED TO THE JEFFERSON COUNTY AIR POL-
    LUTION CONTROL DISTRICT  WITH  1/81  ESTABLISHED AS THE STARTUP DATE FOR AN
    F6D SYSTEM.
I.D. NUMBER   1*9
LOUISVILLE GAS * ELECTRIC
MILL C"EEK NO 3
  <»25  MW - NEW
COAL   3.5- t.O PERCENT SULFUR
AMERICAN AIR FILTER
LIME SCRUBBING
STARTUP  12/77
    out TO THE FACT THAT POWER  DEMAND  HAS  NOT COME UP AS RAPIDLY
    AS HAD BEEN EXPECTED,  START-UP  HAS BEEN MOVLO BACK TO
    DECEMBER 31,1977. CONSTRUCTION  ON  THIS NEW FACILITY'S
    FGO SYSTEM IS APPROXIMATELY  60  PERCENT COMPLETE.
    THIS AAF SYSTEM WILL OPERATE  ON A  CLOSED WATER LOOP
    AND WILL PRODUCE A STABALIZEO SLUDGE.
1.0. NUMBER   50
LOUISVILLE GAS 4 ELECTRIC
MILL CREEK NO 14
  i»25  MW - NEW
COAL   3.5- 4.0 PERCENT SULFUR
AMERICAN AIR FILTER
LIME SCRUBBING
STARTUP   6/60
    DUE TO THE FACT THAI POWER  DEMAND  HAS  NOT COME UP AS
    RAPIDLY AS HAD BEEN EXPECTED,  START-UP HAS CIEEN MOVED
    BACK TO JUNE 1980. THIS  <*2-b-MW  NEW FACILITY WILL
    BE REQUIRED TO COMPLY  WITH  NSPS, FOUNDATION WORK
    is CURRENTLY BEING EFFECTED.  THIS  AAF  SYSTEM WILL
    OPERATE ON A CLOSED WATER LOOP  AND PRODUCE
    STABALIZED SLUDGE.
                                                                 20
                                                                                             PEDCo   ENVIRONMENTAL
                                                                                                    CINCINNATI. OHIO  -452.46

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 COMPANY
           TABLE 2
STATUS OF FGD SYSTEMS DURING
                                                                06/77
 POWER STATION
                       CURRENT MONTH
I.D. NUMBER   51
LOUISVILLE GAS * ELECTRIC
PADDYS RUN NO 6
   65  MW - RETROFIT
COAL 3.5 - H.O PERCENT SULFUR
COMBUSTION ENGINEERING
LIME SCRUBBING
STARTUP   H/73
    REFER TO THE BACKGROUND INFORMATION SECTION IN TABLE 5 OF THIS REPORT.
    THIS SCRUBBING SYSTEM MAS DESIGNED BY COMBUSTION ENGINEERING AND PLACED
    IN SERVICE IN APRIL 1973. PADDYS RUN NO.6 is A PEAK.LOAD UNIT THAT
    OPERATES ONLY DURING DEMAND PERIODS. THE HIGH-CALCIUM VIRGIN LIME STUDY
    BEGAN IN MID-MARCH AND THE FGD SYSTEM DEMONSTRATED 9a» AVAILABILITY UNTIL
    MID-APRIL.  AT THAT TIME SCRUBBING OPERATIONS WERE TEMPORARILY SHUT-
    DOWN BECAUSE THE SCRUBBER CREW WAS REQUIRED AT THE POWER-GENERATING OPER--
    ATIONS.   RESTART IS SCHEDULED FOR MID-JUNE.
I.D. NUMBER   52
MINNESOTA POWER AND LIGHT CO.
CLAY BOSWELL NO. <*
  500  MW - NEW
COAL 0.6 PERCENT SULFUR
PEABODY ENGINEERING
LIME/ALKALINE FLYASH SCRUBBING
STARTUP   0/60
    MINNESOTA P 1 L HAS ANNOUNCED THAT IT HAS SIGNED A LETTER-OF-INTENT WITH
    PEABODY ENGINEERING FOR A LIME/ALKALINE FLYASH S02 CONTROL SYSTEM.
    THE MOST LIKELY CONFIGURATION WILL BE VENTURI SCRUBBERS FOLLOWED BY SPRAY
    TOWERS. EMISSIONS FROM THIS NEWi  COMBUSTION-ENGINEERING BOILER WILL BE
    CONTROLLED TO COMPLY KITH NSPS, THE UNIT WILL FIRE SUB-BITUMINOUS
    COLSTRIP COAL WITH A HEATING VALUE OF 8300 BTU/LB, SULFUR CONTENT OF
    0.8*,  AND ASH CONTENT OF 9.OX. THE START-UP OF COMMERCIAL OPERATIONS
    is SCHEDULED FOR THE SPRING OF i960.
I.D. NUMBER   53
MINNKOTA POWER COOPERATIVE
MILTON R. YOUNG NO. 2
  450  MW - NEW
LIGNITE • 6.500 BTU, 0.7* S
AOL/COMBUSTION EOUIP. ASSOC.
LIME/ALKALINE FLYASH SCRUBBING
STARTUP   8/77
    THE CONTRACT FOR THIS LIME/ALKALINE FLYASH SCRUBBING SYSTEM HAS BEEN
    AWARDED TO AOL/COMBUSTION EQUIPMENT ASSOCIATES.
    DURING THIS REPORTING PERIOD,  THE UTILITY ANNOUNCED THAT CONSTRUCTION
    IS APPROXIMATELY 90* COMPLETE,  AND THAT THE AUGUST 1977 START-UP DATE
    IS STILL GOOD.  THE EMISSION CONTROL SYSTEM WILL  CONSIST OF A COLO-SIDE
    ESP FOLLOWED BY TWO SPRAY TOWERS. MIST ELIMINATION WILL BE EFFECTED BY
    A SIEVE TRAY FOLLOWED BY A CHEVRON M-E. 15X OF THE FLUE GAS WILL BYPASS
    THE SCRUBBER AND BE USED AS REHEAT.
I.D. NUMBER   54
MONTANA POWER CO.
COLSTRIP NO 1
  360  MW - NEW
COAL 0.8 PERCENT SULFUR
AOL/COMBUSTION EOUIP ASSOCIATE
LIME/ALKALINE FLYASH SCRUBBING
STARTUP  10/75
    THE COLSTRIP PLANT IS A MINE MOUTH INSTALLATION.  THE FGD SYSTEM STARTED
    UP IN LATE 1975 AND PROCEEDED THROUGH A SHAKEDOWN AND DEBUGGING OPER-
    ATION PHASE. THE UNIT HAS BEEN OPERATING AT FULL  COMERCIAL CAPACITY.
    THE SCRUBBING SYSTEM DESIGN INCORPORATES VENTURI  WET SCRUBBERS FOR
    PART1CULATE AND SULFUR DIOXIDE REMOVAL. FLUE GAS  CANNOT BE BY-PASSED
    AROUND THE SCRUBBING SYSTEM. INFORMATION AND OPERATING DATA WERE NOT
    MADE AVAILABLE BY THE UTILITY DURING THE REPORT PERIOD.
I.D. NUMBER   55
MONTANA POWER CO.
COtSTRlP NO 2
  360  MW - NEW
COAL 0.8 PERCENT SULFUR
AOL/COMBUSTION EOUIP ASSOCIATE
LIME/ALKALINE FLYASH SCRUBBING
STARTUP   7/76
    THE COLSTRIP PLANT IS A MINE MOUTH FACILITY.  INITIAL OPERATION OF  THE
    SCRUBBING SYSTEM COMMENCED IN JULY 1976.  THIS UNIT  is IDENTICAL TO
    THE. NO.l SYSTEM DESIGN IN THAT THREE SCRUBBLR MODULES ARE INSTALLED FOR
    PARTICULATE AND SULFUR DIOXIDE REMOVAL.  FLUE  GAS CANNOT BE BY-PASSED
    AROUND THE SCRUBBING SYSTEM. INFORMATION  AND  OPERATING DATA WERE NOT
    MADE AVAILABLE BY THE UTILITY DURING THE  REPORT  PERIOD.
                                                                21
                                                                                           PEDCo  ENVIRONMENTAL
                                                                                                  CINCINNATI. OHIO  45246

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 COMPANY
 POWER STATION
                                             TABLE 2
                                  STATUS OF FGO SYSTEMS DURING
                          06/77
                   CURRENT MONTH
1.0. NUMBER   56
MONTANA POWER CO.
COLSTRIP NO, 3
  700  MW - NEW
COAL  0.7 PERCENT SULFUR
ADL/COMBUSTION EQUIP ASSOCIATE
LIME/ALKALINE FLYASH SCRUBBING
STARTUP   7/80
A CONTRACT FOR THE INSTALLATION OF TWO ADDITIONAL LIME/ALKALINE FLYASH
SCRUBBING SYSTEMS HAS BEEN AWARDED TO A.D. LITTLE/COMBUSTION EQUIPMENT
ASSOCIATES. THESE SYSTEMS WILL BE INSTALLED ON UNITS NOS. 3 ANQ «4 OF
THL COLSTRIP POWLK STATION, COLSTRIP UNITS 1 ANO 2 ARE fOTH E3UIPPEO
WITH OPERATIONAL LI ME/ALKALINE FLYASH SCRUBBING SYSTEMS FOR THE REMOVAL
OF PARTICULATES AND SULFUR DIOXIDE. ENGINEERING WORK FOR THE f«EW SYSTEMS
IS NOW UNDERWAY. THIS CONTRACT Is EXPECTED TO EXCEED J50 MM.
I.D. NUMBER   57
MONTANA POWER CO,
COLSTRIP NO. 4
  700  MW - NEW
COAL  0.7 PERCENT SULFUR
ADL/COMRUSTION EQUIP ASSOCIATE
LIME/ALKALINE FLYASH SCRUBBING
STARTUP   7/fll
A CONTRACT FOR THE INSTALLATION OF TWO ADDITIONAL LIME/ALKALINE FLYASH
SCRUBBING SYSTEMS HAS BEEN AWARDED TO A.D. LITTLE/COMBUSTION EQUIPMENT
ASSOCIATES. THESE SYSTEMS WILL BE INSTALLED ON UNITS NOS, 3  AND •* OF
THE COLSTRIP POWER STATION. COLSTRIP UNITS 1 ANO Z ARE BOTH  EQUIPPED
WITH OPERATIONAL LIME/ALKALINE FLYASH SCRUBBING SYSTEMS FOR  THE REMOVAL
OF PARTICULATES ANO SULFUR UIOXIUE. ENGINEERING WORK FOR THE NEW SYSTEMS
IS NOW UNDERWAY. THIS CONTRACT IS EXPECTED TO EXCEED $50 MM.
I.D. NUMBER   58
NEVADA POWER
HARRY ALLEN STATION NO,
  500  MW - NEW
COAL
NOT SELECTED
NOT SELECTED
STARTUP   fc/83
CONSIDERING HOT SIDE ESP IN CONJUNCTION WITH AN FGD SYSTEM,
TIONS HAVE NOT YET BEEN PREPARED.
SPECIFICA-
I.D. NUMBER   59
NEVADA POWER
HARRY ALLEN STATION NO,
  500  MW - NEW
COAL
NOT SELECTED
NOT SELECTED
STARTUP   6/8i»
CONSIDERING HOT SIDE ESP IN CONJUNCTION WITH AN FGD SYSTEM.  SPECIFICA-
TIONS HAVE NOT YET BEEN PREPARED.
I.D. NUMBER   60
NEVADA POWER
HARRY ALLLN STATION NO. 3
  500  MW - NEW
COAL
NOT SELECTED
NOT SELECTED
STARTUP   6/85
CONSIDERING HOT SIDE ESP IN CONJUNCTION WITH AN FGD SYSTEM,
TIONS HAVE NOT YET BEEN PREPARED'
SPECIFICA-
                                                                22
                                                                                            PEDCo  ENVIRONMENTAL
                                                                                                   CINCINNATI. OHIO

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 COMPANY
 POWER STATION
           TABLE 2
STATUS OF FGD SYSTEMS DURING
       06/77


CURRENT MONTH
I.D. NUMBER   61
NEVAOA POWER
HARHY ALLEN STATION NO.
  500  MU • NEW
COAL
NOT SELECTED
NOT SELECTED
STARTUP   6/66
    CONSIDERING HOT SIDE ESP IN CONJUNCTION WITH AN FGD SYSTEM.
    TIONS HAVE NOT YET BEf.U PREPARED.
                                          SPECIFICA-
I.D. NUMBER   62
NEVADA POWER
REID GARDNER NO 1
  125  Mh - RETROFIT
COAL 0.5 - 1.0 PERCENT SULFUR
AOL/COMBUSTION EQUIP ASSOCIATE
SODIUM CARBONATE SCRUBBING
STARTUP   <»/7<»
    REFER TO THE BACKGROUND INFORMATION SECTION IN TABLE 5 OF THIS REPORT.
    THIS SODIUM CARBONATE-BASED JTRONA) SCRUBBING SYSTEM CONSISTS OF ONE
    MODULE CONTAINING A TWIN VARIABLE-THROAT VENTURI SCRUBBER FOLLOWED BY A
    SEPARATOR IN SERIES WITH A SINGLE-STAGE PERFORATED-PLATE ABSORBER TOWER.
    THE MODULE WAS FIRST PLACED IN SERVICE ON BOILER FLUE GAS IN APRIL 197<».
    DURING THE REPORT PERIOD THE SCRUBBER WAS UNAVAILABLE FOR SERVICE BECAUSE
    OF REPAIRS TO DAMAGED LINER MATERIAL. THE SYSTEM is SCHEDULED TO BE BACK
    IN OPERATION BY MID-JUNE.
I.D. NUMBER   63
NEVADA POWER
REID GARDNER NO 2
  125  MW . RETROFIT
COAL 0.5 - 1.0 PERCENT SULFUR
AOL/COMBUSTION E8UIP ASSOCIATE
SODIUM CARBONATE SCRUBBING
STARTUP   i»/7«»
    REFER TO THE BACKGROUND INFORMATION SECTION IN TABLE 5 OF THIS REPORT.
    THIS SODIUM CARBONATE-BASED (TRONA) SCRUBBING SYSTEM CONSISTS OF ONE
    MOUULE CONTAINING A TWIN VARIABLE-THROAT VENTURI SCRUBBER FOLLOWED 8Y A
    SEPARATOR IN SERIES WITH A SINGLE-STAGE PERFORATED-PLATE ABSORBER TOWER.
    THE MODULE WAS FIRST PLACED IN SERVICE ON BOILER FLUE GAS IN APRIL 197<*.
    DURING THE REPORT PERIOD THE SYSTEM WAS IN SERVICE WITH THE EXCEPTION OF
    A 2-wEEK BOILER OUTAGE FOR MAINTAlNENCE AND REPAIRS.
I.D, NUMBER   64
NEVADA POWER
REID GARDNER NO 3
  125  MM - NEW
COAL 0.5 - 1.0 PERCENT SULFUR
AOL/COMBUSTION EQUIP ASSOCIATE
SODIUM CARBONATE SCRUBBING
STARTUP   7/76
    REFER TO THE BACKGROUND INFORMATION SECTION IN TABLE 5 OF THIS REPORT.
    THIS UNIT is A NEW COAL-FIRED BOILER THAT is EQUIPPED WITH SODIUM
    CARBONATE-BASEDITRONA>SCRUB8ING SYSTEM WHICH INCORPORATES A TWIN
    VAKIABLE-THROAT VENTURI SCRUBBER FOLLOWED BY A SEPANATOK IN SERIES WITH
    A SINGLE-STAGE PERFORATED-PLATE ABSORBER TOWER,   THE MODULE WAS FIRST
    PLACED IN SERVICE ON BOILER FLUE GAS IN JULY 1976.  DURING THE PERIOD
    THE SYSTEM WAS OPERATIONAL IN APRIL AND DO«N IN  MAY FOR A S-WEEK OUTAGE
    FOR AN FRP LINER REPLACEMENT IN THE SEPARATOR.
I.D. NUMBER   65
NEVADA POWER
REID GARDNER NO n
  125  MM - NEW
COAL   0-5- 1.0 PERCENT SULFUR
ADL/COMBUSTION EQUIP ASSOCIATE
SODIUM CARBONATE SCRUBBING
STARTUP   O/ 0
    NEVADA POWER COMPANY HAS SIGNED A LETTER OF INTENT WITH COMBUSTION EQUIP-
    MENT ASSOCIATES FOR THE. CONSTRUCTION OF *N FGD SYSTEM ON REID GARDNER NO.

    H,   HOWEVER, CONSTRUCTION OF THE BOILER HAS BEEN INDEFINITELY POSTPONED.
                                                                23
                                                                                          PEDCo  ENVIRONMENTAL
                                                                                                 CINCINNATI OHIO

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 COMPANY
 POWER STATION
           TABLE 2
STATUS OF FGO SYSTEMS DURING
       06/77

CURRENT MONTH
1.0. NUMBER   66
NEVADA POWER
WARNER VALLEY STATION NO.
  250  MW - NEW
COAL
NOT SELECTED
NOT SELECTED
STARTUP   6/82
    SPECIFICATIONS ARE BEING PREPARED FOR A SCRUBBING SYSTEM.
I.D. NUMBER   67
NEVADA POWER
WARNER VALLEY STATION NO. 2
  250  MW • NEW
COAL
NOT SELECTED
NOT SELECTED
STARTUP   6/63
    SPECIFICATIONS ARE BEING PREPARED FOR A SCRUBBING SYSTEM.
I.D. NUMBER   66
NEW ENGLAND ELEC SYSTEM
BRAYTON POINT NO.3
  650  MW - RETROFIT
COAL 3.0 PERCENT SULFUR
NOT SELECTED
REGENERABLE NOT SELECTED
STARTUP   O/ 0
    THE UTILITY IS CURRENTLY INVESTIGATING VARIOUS ADVANCED RE.GENERABLE
    FLUE GAS DESULFURIZftTlON SYSTEMS WHICH OFFER A BREAKTHROUGH IN
    OPERATING COSTS ANO PRODUCE ELEMENTAL SULFUR AS AN ENd
    PRODUCT.  THE UTILITY IS CURRENTLY INVOLVED IN BENCH AND LABORATORY
    SCALE INVESTIGATIONS OF SULFUR RECOVERY.  THE NO. 3 UNIT IS CURRENTLY
    OPERATIONAL,  FIRING LOW SULFUR FUEL OIL.
1,0. NUMBER   69
NIAGARA MOHAWK POWER COOP.
CHARLES R. HUNTLEY NO.6
  100  MW - RETROFIT
COAL 3,5-4,5 PERCENT SULFUR
ATOMICS INTERNATIONAL
AQUEOUS CARBONATE SCRUBBING
STARTUP   6/78
    DURING THE REPORT PERIOD,  CONTRACTS WERE SIGNED AWARDING A CONTRACT
    TO ATOMICS INTERNATIONAL FOK THE DESIGN AND INSTALLATION OF AN AQUEOUS
    CARBONATE FGD SYSTEM. THIS DEMONSTRATION SYSTEM WILL PRODUCE END-PRODUCT
    SULFUR. FUNDS ARE BEING PROVIDED BY THE US EPA AND THE EMPIRE STATE
    ELECTRIC ENERGY RESEARCH CORP. THE DESIGN SOj REMOVAL EFFICIENCY WILL
    BE 90 PERCENT.
I.D. NUMBER   70
NORTHERN INDIANA PUB SERVICE
BAILLY NO. 7
  190  MW - RETROFIT
COAL 3 PERCENT SULFUR
NOT SELECTED
NOT SELECTED
STARTUP   O/ 0
    CONSIDERING A LIME OR LIMESTONE SCRUBBING UNIT.  ALSO WAITING FOH PER-
    FOKMANCE OF WELLMAN LORD/ALLIED CHEMICAL UNIT IN SERVICE AT THEIR
    D.H. MITCHEL NO.H UNIT. LOW SULFUR COAL MAY BE EMPLOYED TO COMPLY WITH
    S02 EMISSION REGULATIONS.
    APPLICABLE INDIANA S02 REGULATIONS ARE STILL NOT FIRMLy ESTABLISHED.
                                                                                          PEDCo  ENVIRONMENTAL
                                                                                                 CINCINNATI. OHIO

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 COMPANY
           TABLE 2
STATUS OF FGD SYSTEMS DURING
06/77
 POWER STATION
                       CURRENT MONTH
I.D. NUMQCR   71
NORTHERN INDIANA PUB SERVICE
BAILLY NO. 8
  i»00  M* - RETROFIT
COAL 3 PERCENT SULFUR
NOT SELECTED
NOT SELECTED
STARTUP   O/ 0
    CONSIDERING A LIME OR LIMESTONE SCRUBBING UNIT.  ALSO WAITING FOR PERFOR-
    MANCE OF WELLMAN LORD/ALLIED CHEMICAL UNIT UNDER CONSTRUCTION AT THEIR
    0. H. MITCHELL NO. 11 UNIT.   LOW SULFUR COAL MAY BE bURNEU TO COMPLY WITH
    S02 EMISSION REGULATIONS.
1.0. NUMBER   72
NORTHERN INDIANA PUB SERVICE
D.H. 1ITCHELL NO.11
  115  MW - RETROFIT
COAL 3.2-3.5 PERCENT SULFUR
DAVY POWERGAS/ALLIED CHEMICAL
WELLMAN LORD/ALLIED CHEMICAL
STARTUP   6/77
    REFER TO THE BACKGROUND INFORMATION SECTION IN TABLE 5 OF THIS REPORT.
    THIS FGO SYSTEM IS AN INTEGRATION OF THE WELLMAN-LORU S02 RECOVERY PROCES
    OFFERED BY UAVY POWERGAS AND THE S02 TO SULFUR REDUCTION PROCESS DE-
    VELOPED BY ALLIED CHEMICAL,  DAVY POHERGAS IS THE DESIGN AND CONSTRUCTION
    FIRM AND ALLIED CHEMICAL IS  SYSTEM OPERATOR AND PRODUCT MARKETER.
    DURING THE REPORT PERIOD THE DEMONSTRATION SCRUBBER PLANT WAS STARTED UP
    ANU OPERATED AT APPROXIMATELY 60 PERCENT FLUE GAS CAPACITY BECAUSE OF
    AIR PREHEATER PROBLEMS IN THE BOILER.
I.D. NUMBER   73
NORTHERN STATES POWER CO.
SHERBURNE COUNTY STATION NO.l
  710  MW - NEW
COAL 0.8 PERCENT SULFUR
COMBUSTION ENGINEERING
LIMESTONE SCRUBBING
STARTUP   3/76
    REFER TO THE BACKGROUND INFORMATION SECTION IN TABLE 5 OF THIS REPORT.
    FULL COMMERCIAL OPERATION OF THE SYSTEM BEGAN ON MAY 1, l976t THE SCRUB-
    BING SYSTEM FO* THIS UNIT CONSISTS OF 12 MODULES. EACH SCRUBBING MODULE
    INCORPORATES A VENTuRI-ROO SECTION AND A MARBLE BED ABSORBER FOR PAR-
    TICULATE AND SULFUR DIOXIDE REMOVAL.  AVAILABILITY INDEX VALUES FOR
    THE MONTHS OF APRIL AND MAY WERE 95 AND 92 PERCENT, RESPECTIVELY. THE
    UNIT WAS TAKEN OUT  OF SERVICE IN MID-MAY FOH A SCHEDULED TURBINE/BOILER
    OVERHAUL. RESUMPTION OF OPERATIONS IS SCHEDULED FOR MID-JUNE.
I.D. NUMBER   7U
NORTHERN STATES POWER CO,
SHERBURNE COUNTY STATION NO.2
  680  MW - NEW
COAL 0.6 PERCENT SuLFuR
COMBUSTION ENGINEERING
LIMESTONE SCRUBBING
STARTUP   t»/77
    REFER TO THE BACKGROUND INFORMATION SECTION IN TABLE 5 OF THIS REPORT.
    THL SHERBURNE NO.2 AIR QUALITY CONTROL SYSTEM IS IDENTICAL IN DESIGN TO
    THE SYSTEM IN OPERATION ON THE NO.l UNIT AT THIS STATION. TWELVE 2-STAGE
    PAKT1CULATE SCRUBBER (VENTURI-ROD SCRUBBER) AND SULFUR DIOXIDE ABSORBER
    (MARBLE-BED ABSORBER)  MODULES ARE PROVIDED FOR FLY ASH AND S02 CONTROL.
    ELEVEN MODULES ARE REQUIRED FOR HULL GENERATING CAPACITY OPERATIONS.
    TOTAL SYSTEM AVAILABILITY INDEX VALUES REPORTED FOR THE MONTHS OF APRIL
    AND MAY WERE 92 AND 91 PERCENT, RESPECTIVELY.
I.D. NUMBER   75
NORTHERN STATES POWER CO.
SHERBURNE COUNTY STATION NO.3
  860  Mw - NEW
COAL 0.8 PERCENT SULFUR
NOT SELECTED
NOT SELECTED
STARTUP   5/81
    NSP HAS ANNOUNCED THAT TWO ADDITIONAL COAL-FIRED POWER-GENERATING UNITS
    ARE SCHEDULED TO BE  INSTALLED AT THEIR SHERBURNE COUNTY GENERATING
    STATION IN BECKER, MINNESOTA. COMMERCIAL OPERATION DATES ARE NOW
    SCHEDULED FOR MAY 1981 AND MAY 1983.  EACH UNIT IS NOMINALLY RATED AT
    660 MW. THE UTILITY  IS CURRENTLY REUUESTING/EVAtUATING BIDS FOR THE
    FGD SYSTEM. THE  BOILER CONTRACT HAS BEEN AWARDED TO BABCOCK AND
    WILCOX  AND THE TURBINE WILL BE SUPPLIED BY GENERAL ELECTRIC.
                                                                                           PEDCo  ENVIRONMENTAL
                                                                                                  CINCINNATI. OHIO 45246

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 COMPANY
           TABLE 2
STATUS OF FGD SYSTEMS DURING  06/77
 POWER STATION
                       CUKRENT MONTH
1.0, NUMBER   76
NORTHERN STATES POWER CO.
SHERBURNE COUNTY STATION NO,
  660  MW • NEW
COAL 0.8 PERCENT SULFUR
NOT SELECTED
NOT SELECTED
STARTUP   5/83
    NSP HAS ANNOUNCED THAT TWO ADDITIONAL COAL-FIRED POwER-GENERATING UNITS
    ARE SCHEDULED TO BE INSTALLED AT THEIR SHERBURNE COUNTY GENERATING
    STATICS IN BECKER, MINNESOTA, COMMERCIAL OPERATION UATES ARE NOW
    SCHEDULED FOR MAY 1981 AND MAY 1983. EACH UNIT IS NOMINALLY RATED AT
    860 MW, THE UTILlTy IS CURRENTLY REQUESTING/EVALUATING BIOS FOR THE
    FGU SYSTEM. THE BOILER CONTRACT HAS BEEN AWARDED TO BABCOCK AND
    WILCOX AND THE TURBINE WILL BE SUPPLIED BY GENERAL ELECTRIC.
I.D. NUMBER   77
OTTER TAIL POWER COMPANY
COYOTE NO. 1
  1400  MM - NEW
LIGNITE 0.9 PERCENT SULFUR
NOT SELECTED
HOT SELECTED
STARTUP   5/81
    THIS NEW COAL-FIRED STATION IS JOINTLY OWNED BY FIVE UTILITIES, OTTER
    TAIL POWER is THE MAJOR OWNER AND CONSTRUCTOR. MONTANA-UAKOTA UTILITIES
    is THE FACILITY OPERATOR. THIS PLANNED UNIT WILL FIRE LOW SULFUR LIGNITE
    FROM THE MERCER COUNTY AREA. THE UTILITY is NOW INVESTIGATING VARIOUS
    EMISSION CONTROL STRATEGIES TO MEET PARTICULATE AND SULFUR DIOXIDE
    COOES. SULFUR DIOXIDE REMOVAL STRATEGIES BEING CONSIDERED AT THE PRESENT
    INCLUDE WLT REMOVAL PROCESSES AND DKY NAHCOLITE INJECTION COLLECTED
    ON FABRIC FILTERS. THIS <»OO-MW UNIT WILL BE A B*W  CYCLONE-FIRED BOILER.
I.D. NUMBER   78
PACIFIC POWER AND LIGHT CO.
JIM BRIOGER NO. i»
  509  MW - NEW
COAL 0.56 PERCENT SULFUR(AVG.)
UNIVERSAL OIL PRODUCTS
SODIUM CARBONATE SCRUBBING
STARTUP   9/79
    THE UTILITY IS CONTINUING PILOT PLANT WORK DESIGNED TO FINALIZE FGD
    SYSTEM OPERATING PARAMETERS. CURRENT TESTING IS CENTLHEO AROUND DETER-
    MINATION OF SPRAY NOZZLE CONFIGURATION. FOLLOWING THL SPRAY NOZZLE
    EVALUATION, THE TESTING WILL PROCEED INTO A PERIOD OF DETERMINING EFFECTS
    OF L/G, PH, AND GAS FLOW RATE, SUBSEQUENT TESTS WILL BE AIMED AT MINIMI-
    ZING MIST ENTRAINMLNT. CURRENT PLANS INCLUDt THE USE OF COOLING TOWER
    SLOWDOWN AS THE SOURCE OF MAKEUP WATER. THE WLT/DRY STACK wILL HAVE A
    CEILCOTE LINING.
1.0. NUMBER   79
PENNSYLVANIA POWER CO.
BRUCE MANSFIELD NO. 1
  835  MW - NEW
COAL H.l PERCENT SULFUR
CHEMICO
LIME SCRUBBING
STARTUP   1/76
    REFER TO THE BACKGROUND INFORMATION SECTION IN TABLE 5 OF THIS REPORT.
    THIS EMISSION CONTROL SYSTEM IS CAPABLE OF REMOVING FLYASH AND S02 FROM
    3.35 MM ACFM OF FLUE GAS VIA WET LI«E SCRUBBING. THL INITIAL SHAKLOOWN
    ANU DEBUGGING PHASE OF OPERATION BEGAN FOR PART OF THE SYSTEM IN DECEMBER
    1975. FULL COMMERCIAL OPERATION COMMENCED IN APRIL 1976. TO DATE, ALL 6
    OF THE SCRUBBING TKAINS HAVE BEEN SUCCESSFULLY PUT INTO OPERATION.
    THt AVAILABILITY INDEX VALUE FOR THE ENTIRE SCRUBBING SYSTEM HAS
    BEEN IN THE MID-90 PERCENT RANGE SINCE COMMERCIAL START-UP.
I.D. NUMBER   80
PENNSYLVANIA POWER CO.
BRUCE MANSFIELD NO. 2
  835  Mw - NEW
COAL H.7 PERCENT SULFUR
CHEMICO
LIME SCRUBBING
STAKTUP  10/77
    THE FGD SYSTEM FOR THIS INSTALLATION WILL BE A CHEMICO WET LIME SCRUBBING
    SYSTEM CAPABLE OF REMOVING PARTICULATE MATTER AND 502 FROM THE FLUE GAS.
    THIS SYSTEM IS CURRENTLY UNfjER CONSTRUCTION. INITIAL FGD SYSTEM START-
    UP IS NOW SCHEDULED FOR EARLY JULY, FOLLOWING A 3-MONTH SHAKEDOWN
    PERIOD, THE UTILITY is SCHLOULING COMMERCIAL OPERATION FOR OCTOBER
    1977.
                                                                26
                                                                                           PEDCo  ENVIRONMENTAL
                                                                                                  CINCINNATI. OHIO

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 COMPANY

 POWER STATION
           TABLE 2
STATUS OF FGD SYSTEMS DURING
06/77
                       CURRENT MONTH
I.D. NUMBER   81
PENNSYLVANIA POWER CO.
BRUCE MANSFIELD NO. 3
  835  MW - NEW
COAL «».7 PERCENT SULFUR
PULLMAN KELLOSG
LIME SCRUBBING
STARTUP   <+/80
    THE PULLMAN KELLOGG DIVISION OF PULLMAN INCORPORATED HAS BEEN
    AWARDED A CONTRACT IN EXCESS $50 MILLION BY THE CAPCO CONSOHTIUM
    FOR THE INSTALLATION OF SULFUR DIOXIDE SCRUBBER ON THIS 835 MW COAL-
    FIREO POWER-GENERATING UNIT.  THE EMISSION CONTROL SYSTEM FOR THIS
    UNIT WILL CONSIST OF ESP'S UPSTREAM OF WEIR HORIZONTAL CROSSFLOW WET
    SCRUBBING MODULES. CONSTRUCTION OF THE BOILER is CURRENTLY IN PROGRESS.
    DUL TO REVISED CAPCO LOAD FORECASTS, UNIT START-UP HAS BEEN MOVED
    BACK TO 0"*/60.
I.D. NUMBER   82
PHILADELPHIA ELECTRIC CO.
CROMBY
  150  MW - RETROFIT
COAL   2-H PERCENT SULFUR
UNITED ENGINEERS / PECO
MAGNESIUM OXIDE SCRUBBING
STARTUP   6/80
    THE. UTILITY PLANS TO RETROFIT ONE OF THE TWO BOILERS AT CROMBY WITH  AN
    FGU SYSTEM. HOWEVER. A FINAL DECISION HAS NOT BEEN MAUL.  THE PROCESS
    BEING GIVEN PRIME CONSIDERATION IS MAGNESIUM OXIDE SCRUBBING DESIGNED
    JOINTLY BY UNITED ENGINEERS AND PHILADELPHIA ELECTRIC.  ENGINEERING
    DESIGN WORK IS SCHEDULED TO COMMENCE IN 1977. TENTATIVE FGD SYSTEM
    START-UP IS SCHEDULED FOR JUNE 1980.
I.D. NUMBER   83
PHILADELPHIA ELECTRIC CO.
EODYSTONE NO. 1A
  120  MW - RETROFIT
COAL 2.5 PERCENT SULFUR
UNITED ENGINEERS / PECO
MAGNESIUM OXIDE SCRUBBING
STARTUP   9/75
    REFER TO THE BACKGROUND INFORMATION SECTION IN TABLE 5 OF THIS REPORT.
    THE EMISSION CONTROL SYSTEM FOR THIS UNIT CONSISTS OF THREE PARALLEL
    SCRUbBING TRAINS FOR THE CONTROL OF PARTICULATE AND SULFUR UIOXIOE.
    THL C-SIUE SCRUBBING TRAIN INCLUDES AN S02 ABSORBER MODULE IN SERIES
    WITH A PARTICULATE SCRUBBER.  APPROXIMATELY ONE-THIRD OF THE BOILER FLUE
    GAS is SCRUBBED WITH MAGNESIUM OXIDE SLURRY FOR 502 REMOVAL. THE SPENT
    SLURRY IS REGENERATED AT THE  ESSEX SULFURIC ACID PLANT IN NEWARK. N.J.
    THE REGENERATED MAGOX IS RETURNED TO THE PLANT FOR S02 SCRUBBING SERVICE.
I.D. NUMBER   8V
PHILADELPHIA ELECTRIC CO.
EDDYSTONE NO. IB
  2<»o  MW - RETROFIT
COAL 2.5 PERCENT SuLFuR
UNITED ENGINEERS / PECO
MAGNESIUM OXIDE SCRUBBING
STARTUP   6/80
    THE INSTALLATION OF S02 SCRUBBERS ON THE BALANCE OF THE FLUE GAS FROM
    THIS UNIT WILL FOLLOW PENDING THE OUTCOME 0^ THE PERFORMANCE OF THE
    SCRUBBING UNIT WHICH HAS BLEN INSTALLED AND INTERMITTENTLY OPERATIONAL
    ON THE EDDYSTONE NO.l UNIT. CURRENTLY. 3 WET PARTICULAR SCRUBBERS ARE
    SERVICE ON THIS UNIT,
I.D. NUMBER   85
PHILADELPHIA ELECTRIC CO.
EDDYSTONE NO. 2
  336  MW - RETROFIT
COAL 2.«» PERCENT SULFUR
UNITED ENGINEERS / PECO
MAGNESIUM OXIDE SCRUBBING
STARTUP   6/80
    THE UTILITY IS AWAITING PERFORMANCE RESULTS FROM THE EXISTING MAGOX
    SCRUBBER INSTALLED ON UNIT NO.I AT THIS STATION BEFORE PROCEEDING
    WITH THE DESIGN OF AN FGo SYSTEM FOR THIS COAL-FIRE.U BOILER. THE PROCESS
    BEING GIVEN PRIME CONSIDERATION IS MAGNESIUM OXIDE SCRUBBING DESIGNED
    JOINTLY BY UNITED ENGINEERS AND PHILADELPHIA ELECTRIC. ENGINEERING
    DESIGN WORK IS SCHEDULED TO COMMENCE IN 1977.  TENTATIVE FGD SYSTEM
    START-UP is SCHEDULED FOR JUNE i960.
                                                                27
                                                                                           PEDCo  ENVIRONMENTAL
                                                                                                  CINONNAT,. OHIO .45246

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 COMPANY
           TABLE: 2
STATUS OF FGD SYSTEMS DURING
06/77
 POWER STATION
                       CUKRENT MONTH
1.0. NUMBER   86
POTOMAC ELECTRIC S POWER
DICKERSON NO.l
  190  Mw - RETROFIT
COAL
CHEMICO
NOT SELECTED
STARTUP   0/78
    THE UTILITY HAS AWARDED A CONTRACT TO CHEMICO AIR POLLUTION FOR THE
    INSTALLATION OF A WET SCRUBBING SYSTEM ON THIS UNIT, THE SCKUBBER
    CONSISTS OF A SINGLE MODULE DOUBLE VENTURI THROAT UKIT. THE FlKST
    VENTURI STAGE IS DESIGNED FOR REMOVAL OF PAHT1CULATE HATTEH ONuT. THE
    SECOND VENTuRI STAGE WILL BE INSTALLED FOR FgTuRE CONSIDERATIONS IF
    THE UTILITY ELECTS TO SCRUB SULFUR DIOXIDE. THE DESIGN ALLOWS CON-
    SIDERATION FOR EITHER A REGENERATIVE OR NON-HEGENERAT1VE ^GQ SYSTEM,
    FINAL DECISIONS ARE NOT EXPECTED UNTIL EARLT 1979.
1.0. NUMBER   87
POTOMAC ELECTRIC 4 POWER
OICKERSON NO,2
  190  MW - RETROFIT
COAL
CHEMICO
NOT SELECTED
STARTUP   0/78
    THE UTILITY HAS AWARDED A CONTRACT TO CHEMICO AIR POLLUTION FOR THE
    INSTALLATION OF A WET SCRUBBING SYSTEM ON THIS UNIT, THE SCRUBBER
    CONSISTS OF A SINGLE MODULE DOUBLE VENTURI THROAT UNIT. THE FIRST
    VENTURI STAGE is DESIGNED FOR REMOVAL OF PARTICULATE MATTER ONLY. TH
    SECOND VENTURI STAGE WILL 6E INSTALLED FOR FUTURE CONSIDERATIONS IF
    THE UTILITY ELECTS TO SCRUB SULFUR DIOXIDE. THE DESIGN ALLOWS CON-
    SIDERATION FOR EITHER A REGENERATIVE OR NON-REGENEKATIVE FGD SYSTEM,
    FINAL DECISIONS ARE NOT EXPECTED UNTIL EARLY 1979.
I.O.  NUMBER   88
PUBLIC SEHVICE CO OF NEW HEX.
SAN JUAN NO. 1
  375  Mw - NEW
COAL    0.8 PERCENT SULFUR
DAVY  POWERGAS/ALLIED CHEMICAL
WELLMAN LORD/ALLIED CHEMICAL
STARTUP  11/77
    THE CONSTRUCTION OF THIS SYSTEM IS NOW UNDERWAY. CONSTRUCTION IS
    CUKRENTLY APPROXIMATELY 30 PERCENT COMPLETE. START-UP IS NOW SCHEDULED
    FOK NOV. 1977. THIS FGD SYSTEM IS AN INTERbRATlON OF THE WLLLMAN LORD
    S02 RECOVERY PROCESS OF DAVY POWERGAS AND ALLIED CHEMICAL'S S02 RE-
    DUCTION TO SULFUR PROCESS. A HOT SIDE ELECTROSTATIC PRECIPlTAToR WILL
    PRECEDE THE SCRUBBING UNIT. FOUR ABSORBER TOWERS WILL BE INSTALLED
    FOR LACH UNIT. THREE WILL CARRT THL FULL LOAD. MOLTEN SULFUK WILL BE
    STORED ON THE PLANT SITE.
I.D. NUMBER   89
PUBLIC SERVICE CO OF NEW MEX.
SAN JUAN NO. 2
  3"»0  Mw - RETROFIT
COAL   0,8 PERCENT SULFUR
DAVY POWERGAS/ALLIED CHEMICAL
WELLMAN LORD/ALLIED CHEMICAL
STARTUP  11/77
    THE CONSTRUCTION OF THIS SYSTEM IS NOW UNDERWAY. CONSTRUCTION IS
    CUKRENTLY APPROXIMATELY 30 PERCENT COMPLETE. START-UP IS NOW SCHEDULED
    FOrt NOV. 1977. THIS FGD SYSTEM IS AN INTERGKAUON OF THE w^LL^AN LO«D
    502 RECOVERY PROCESS OF OAvY POWERGAS AND ALLIED CHEMICAL'S S02 RE-
    DUCTION TO SULFUR PROCESS. A HOT SIDE ELECTROSTATIC PRECIPITATQR WILL
    PRt-CEDE THE SCRUBBING UNIT. FOUR ABSORBER TOWERS WILL BE INSTALLED
    FOR LACH UNIT. THREE WILL CARRY THE FULL LOAD. MOLTE.N SULFUR WILL BE
    STORED ON THE PLANT SITE.
I.O. NUMBER   90
PUBLIC SEHVICE CO OF NEW MEX.
SAN JUAN NO. 3
  500  MW - NEW
COAL 0.8 PERCENT SULFUR
NOT SELECTED
REGENERABLE NOT SE.LECTEO
STARTUP   1/79
    THE UTILITY HAS SIGNED A LETTEH-OF-INTENT WITH DAVY POWERGAS FOR
    ONL SCRUBBER MODULE WHICH WILL BE DESIGNED TO BRING THE UNIT INTO
    COMPLIANCE WITH NSPS BY JAN. 1979. THE FGO SYSTEM FOR THE REMAINDER
    OF THE FLUE GAS FROM THIS 500-MW UNIT HAS NOT BEEN SELECTED. PRIMARY
    PARTICIPATE CONTROL WILL BL EFFECTED BY AN UPSTREAM LSP.
                                                                                           PEDCo  ENVIRONMENTAL
                                                                                                  CINCINNATI. OHIO 45246

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 COMPANY
           TABLE 2
STATUS OF FGD SYSTEMS DURING  Ob/77
 POWER STATION
                       CUKHENT MONTH
I.D. NUMBER   91
PUBLIC SLHVICE CO OF NEW MEX,
SAN JUAN NO. 4
  500  MW - NEW
COAL O.B PERCENT SULFUR
NOT SELECTED
REGENERABLE NOT SELECTED
STARTUP   5/81
    THE UTILITY MAS PLACED A HOLD ON FURTHER ENGINEERING DESIGN WORK AT THE
    PRESENT TIME.  THE PROJECTED START-UP DATE FOR UNIT 4 IS
    MAY 1981.  THE  WELLMAN LORD AND OTHE« SULFUR DIOXIDE HLCOVEHY PROCESSES
    ARL NOW UNDER  CONSIDERATION BY THE UTILITY. AN ESP WILL BE PROVIDED
    UPSTREAM OF THE FGU SYSTEM FOR PRIMARY ^ARTICULATE CUNTHOL.
1,0. NUMBER   92
PUBLIC SERVICE OF INDIANA
GIBSON NO. 3
  650  MW - NEW
COAL 3.3 PERCENT SULFUR
NOT SELECTED
NOT SELECTED
STARTUP   0/78
    THE UTILITY  HAS COMPLETED THE  EVALUATION OF BID SPECIFICATIONS
    SUBMITTED FOR FGD SYSTEMS FOK  ROTH UNITS 3 AND 4 AT THIS STATION.
    NO DECISION  HAS YET BEEN MADE.
I.D. NUMBER   93
PUBLIC SERVICE OF INDIANA
GIBSON NO. 4
  650  MW • NEW
COAL 3.3 PERCENT SULFUR
NOT SELECTED
NOT SELECTED
STARTUP   0/79
    THE UTILITY HAS COMPLETED THE EVALUATION OF  BIO SPECIFICATIONS
    SUBMITTED FOR FGD SYSTEMS FOR BOTH UNITS 3 AND if AT THIS STATION.
    NO DECISION HAS YET BELN MAUE.
I.D. NUMBER   94
SALT RIVER PROJECT
CORONADO NO.l
  350  MU - NEW
COAL 1.0 PERCENT SULFUR (MAX)
PULLMAN KELLOGG
LIMESTONE SCRUBBING
STARTUP   4/79
    THIS NEW UNIT WILL BURN LOW SULFUR  WESTERN COAL.  A MAXIMUM OF 60* OF THE
    FLUE GAS WILL BE SCRUBBED TO MEET  SULFUR  DIOXIDE  EMISSION REGULATIONS.
    PULLMAN/KELLOGG WILL DESIGN AND FABRICATE TWO WEIR HORIZONTAL
    CROSSFLOW SCRUBBER MODULES. WHICH  WILL UTILIZE LIMESTONE  SLURRY  FOR
    S02 CONTROL.  THE SYSTEM WILL UTILIZE  RUBBER-LINED SLURRY  RECYCLE PUMPS.
    EACH RATED AT 9300 GPM, RIGIFLAKE-LINED SCRUBBER  MODULES, VERTICAL HEIL
    DEMISTERSt AND A MINIMUM OF 20  PLRCENT REHEAT. A  SLUDGf  DISPOSAL STRATEGY
    HAS NOT BEEN  FINALIZED? BUT SLUDGE  WILL BE EITHER PONDCU  OH FIXATED.
I.D. NUMBER   95
SALT RIVEN PROJECT
CORONADO NO.2
  350  MW - NEW
COAL i.o PERCENT SULFUR 
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 COMPANY

 POWER STATION
           TABLE 2
STATUS OF FGD SYSTEMS DURING  06/77

                       CURRENT MONTH
1,0. NUMBER   96
SALT RIVER PROJECT
CORONAOO NO.3
  350  MW . NEW
COAL 1.0 PERCENT SULFUR (MAX)
NOT SELECTED
LIMESTONE SCRUBBING
STARTUP   0/87
    THIS NEW UNIT WILL BURN LOW SULFUR WESTERN COAL. 80 PERCENT OF THE
    GAS HILL BE SCRUBBED TO MEET SULFUR DIOXIDE EMISSION RESULATIONS.
    THE UTILITY IS CURRENTLY CONSIDERING THE INSTALLATION OF T*0 HORIZONTAL
    CROSSFLOW SCRUBBING MODULES EMPLOYING A LIMESTONE SCRUBBING SOLUTION
    TO REMOVE, soj FROM THE FLUE GAS,  SCHEDULED COMMERCIAL OPERATION
    DATE IS 1987.  PLANS FOR AN EMISSION CONTROL SYSTEM HAVE <<(OT
    BEEN FINALIZED.
I.D. NUMBER   97
SOUTH CAROLINA PUBLIC SERVICE
WINYAH NO. 2
  280  MW . NEW
COAL  1.0 PERCENT SULFUR
BABCOCK ft WILCOX
LIMESTONE SCRUBBING
STARTUP   7/77
    BOILER START-UP HAS BEEN DELAYED* DUE TO THE DELAY IN THE DELIVERY
    OF THREE RELAYS. ALL OTHER EQUIPMENT IS ON-SITE, INSTALLED AND PREPARED
    FOR START-UP. THE BjW LIMESTONE FGD SYSTEM WILL SCRUB 50 PERCENT OF THE
    FLUE GAS, REMOVING 69 PERCENT OF THE SCRUBBER INLET SO?. RUBBER LIVING
    WILL BE A FEATURE OF THE SLURRY PREP TANK, RETENTION TANK. AND THE SLURRY
    RECYCLE PUMPS. THE STACK FEATURES AN FRP LINING, THE UNSTABILIZED SLUDGE
    WILL BE DISPOSED IN AN UNLINED 20-YEAR CAPACITY POND.
I.D. NUMBER   98
SOUTHERN ILLINOIS POWER CO OP
MARION NO. i»
  18H  MU - NEW
COAL   <*.5-5.0 PERCENT SULFUR
BABCOCK ft WILCOX
LIMESTONE SCRUBBING
STARTUP   6/78
    CONSTRUCTION HAS BEGUN ON THIS 18H-MU UNIT AND FGD SYSTEM, WITH FOUNDA-
    TION WORK COMPLETED AND PRECIPITATOR INSTALLATION UNDERWAY,  TOTAL CAPI-
    TAL COST FOR THE SCRUBBING SYSTEM IS REPORTED AS $10,000,000, OR «5t»/KW.
    THIS FIGURE INCLUDES THE TWO SPHAY TOWERS, AND ALL ANCILLARY EUUIPMENT.
    THIS FIGURE DOES NOT INCLUDE THE E.S.P. OR CONSTRUCTION COSTS. SIPc IS
    NOT PLANNING TO UTILIZE FLUE GAS REHEAT AND IS CURRENTLY PLANNING ON
    INCORPORATING A CEILCOTE LINING IN THE STACK,  NINETY PERCENT OF THE NEC-
    ESSARY EQUIPMENT IS ON-SITE AS OF THIS REPORT PERIOD.
I.D. NUMBER   99
SOUTHERN INDIANA GAS4ELECTRIC
A.B. BROWN NO.i
  250  MW . NEW
COAL 3.75 PERCENT SULFUR
FMC CORPORATION
DOUBLE ALKALI SCRUBBING
STARTUP   4/79
    THIS NEW COAL-FIRED POWER-GENERATING UNIT IS PART OF A NEW GENERATING
    STATION LOCATED IN WEST FRANKLIN,INDIANA,  THE SYSTEM WILL PRODUCE FIL-
    TER CAKES AS A WASTE PRODUCT WHICH WILL BE DISPOSED OF IN AN ONSITE
    LANDFILL. A BUELL-ENVIHOTECH ESP WILL CONTROL PARTICULATE
    EMISSIONS.  THE UTILITY HAS AWARDED A CONTRACT TO FMC FOR THE
    INSTALLATION OF A DOUBLE ALKALI SCRUBBING SYSTEM UTILIZING SODA ASH
    ANU LIME.  FGD SYSTEM CONSTRUCTION IS SCHEDULED TO BEGIN IN THE FALL
    OF 1977,  START-UP IS SCHEDULED FOR 0<«/79.
I.D. NUMBER  100
SOUTHERN MISSISSIPPI ELECTRIC
R.D. MORROW NO.I
  100  MU - NEW
COAL i.o PERCENT SULFUR
RILEY STOKER / ENVIRONEERING
LIMESTONE SCRUBBING
STARTUP  11/77
    THIS NEW COAL-FIRED UNIT WILL FIRE 1,0 PERCENT SULFUR COAL. A CONTRACT
    HAS BEEN AWARDED TO RILEY STOKER/ENVIRONEERING FOR THE INSTALLATION OF
    A WET LIMESTONE SCRUBHING SYSTEM. PARTICULATES WILL BE CONTROLLED 3Y A
    HIGH-EFFICIENCY ESP UPSTREAM OF THE SCRUBBING SYSTEM. DESIGN SULFUR
    DIOXIDE AND PARTICULATE REMOVAL EFFICIENCIES ARE as AND 99.6 PERCENT,
    RESPECTIVELY. SCRUBBER SLUUGE WILL HE STABILIZED WITH FLYASH AND DISPOSED
    ON THE PLANT SITE.  CONSTRUCTION OF THE SCRUBBING SYSTEM is NOW IN
    PROGRESS.  ERECTION OF THE ABSORBER TOWERS HAS BEEN COMPLETED.
                                                                30
                                                                                           PEDCo  ENVIRONMENTAL
                                                                                                  CINCINNATI. OHIO

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 COMPANY
           TABLE 2
STATUS OF FGC SYSTEMS DURING
                                                                06/77
 POWER STATION
                       CURRENT MONTH
1.0. NUMBER  101
SOUTHERN MISSISSIPPI ELECTRIC
R.D. MORROW NO.2
  160  MW - NEW
COAL 1.0 PERCENT SULFUR
RILEY STOKER / ENV1RONLERING
LIMESTONE SCRUBBING
STARTUP   6/78
    THIS NEW COAL-FIRED UNIT WILL FIRE 1.0 PERCENT SULFUR COAL. A CONTRACT
    HAi> BEEN AWARDED TO RILEY STOKER/ENVIRONEERING FOR THE INSTALLATION OF
    A WET LIMESTONE SCRUBBING SYSTEM. PARTICULARS WILL BE CONTROLLED BY A
    HIGH.EFFICIENCY ESP UPSTREAM OF THE SCRUBBING SYSTEM. DESIGN SULFUR
    DIOXIDE AND PARTICULATE REMOVAL EFFICIENCIES ARE 85 AND 99.6 PERCENT.
    RESPECTIVELY. SCRUBBER SLUDGE WILL BE STABILIZED WITH FLYASH AND DISPOSED
    ON THE PLANT SITE. ERECTION OF THE ABSORBER TOWERS IS NOW IN PROGRESS.
I.D. NUMBER  102
SPRINGFIELD CITY UTILITIES
SOUTHWEST NO. 1
  200  MW - NEW
COAL 3.5 PERCENT SULFUR
UNIVERSAL OIL PRODUCTS
LIMESTONE SCRUBBING
STARTUP   <»/77
    THE SCRUBBER BECAME OPERATIONAL ON A TRIAL BASIS IN EARLY APRIL.  COMMER-
    CIAL OPERATION IS SLATED BY 6/15,  THE SYSTEM IS EXPERIENCING DEMlSTER
    SCALING AND SOME CONTROL PROBLEMS.  ALSO CORROSION OF THE PRESATURATOR
    HAS TAKEN PLAcE AND RE-LINING APPEARS NECESSARY.  NO DEFINITE EFFICIENCY
    TESTS HAVE BEEN MADE AS YET DUE TO THE EFFECTS OF THESE PROBLEMS.  THE
    TOP PORTION OF THE STACK AND BKEECHING ARE CEILCOTE LINED.
I.D. NUMBER  103
TENNESSEE VALLEY AUTHORITY
SHAWNEE N0.10A
   10  MW - RETROFIT
COAL 2.9 PERCENT SULFUR
UNIVERSAL OIL PRODUCTS
LIME/LIMESTONE SCRUBBING
STARTUP   <»/72
    REFER TO BACKGROUND INFORMATION SECTION IN TABLE 5 OF THIS REPORT. THIS
    TUKBULENT CONTACT ABSORBER(TCA> LIME/LIMESTONE SCRUBBING SYSTEM HAS BEEN
    OPERATIONAL SINCE APRIL 1972. THIS TEST PROGRAM IS FUNDED BY THE EPA.
    TVA IS THE CONSTRUCTOR AND FACILITY OPERATOR. THE BECHTEL CORP. OF SAN
    FRANCISCO IS THE MAJOR CONTRACTOR. TEST DIRECTOR, ANU REPORT WRITER.
I.D. NUMBER  104
TENNESSEE VALLEY AUTHORITY
SHAWNEE N0.10B
   10  MW . RETROFIT
COAL 2.9 PERCENT SULFUR
CHEMICO
LIME/LIMESTONE SCRUBBING
STARTUP   i»/72
    REFER TO BACKGROUND INFORMATION SECTION IN TABLE 5 OF THIS REPORT. THIS
    VENTURI/SPRAY TOWER LIML/LIME.STONE. SCRUBBING SYSTEM HAS BEEN OPERATIONAL
    SINCE APRIL 1972. THIS TEST PROGRAM IS FUNDED BY THE EPA. TVA IS THE
    CONSTRUCTOR AND FACILITY OPERATOR. THE BECHTEL CORP. OF SAN FRANCISCO IS
    THE MAJOR CONTRACTORiTEST DIRECTOR. AND REPORT WHITER.
I.D. NUMBER  105
TENNESSEE VALLEY AUTHORITY
WIDOWS cREEK NO. e
  550  MW - RETROFIT
COAL   3.7 PERCENT SULFUR
TENNESSEE VALLEY AUTHORITY
LIMESTONE SCRUBBING
STARTUP   5/77
    REFER TO THE BACKGROUND INFORMATION SECTION IN TABLE 5 OF THIS REPORT.
    THE EMISSION CONTROL SYSTEM FOR THIS 550-MW COAL-FIRED POWER-GENERATING
    UNIT CONSISTS OF EXISTING ELECTROSTATIC PRE.CIPITATORS FOLLOWED B* FOUR
    PARALLEL SCRUBBING TRAINS, EACH CAPABLE OF HANDLING 25 PERCENT OF THE
    BOILER FLUE GAS FROM UNIT NO.  8. INITIAL OPERATION OF THE SCRUBBER PLANT
    OCCURRED ON MAY 16.  FLUE GAS WAS PASSED THROUGH TWO (TRAINS A AND B)  OF
    THE 14 TRAINS, FLUSHING AND CLEANOUT OF THE REMAINING 2 TRAINS IS STILL IN
    PROGRESS.  BOILER CAPACITY WAS  APPROXIMATELY 50 PERCENT OF FULL LOAD,
                                                                                           PEDCo   ENVIRONMENTAL.
                                                                                                  CINCINNATI. OHIO 45246

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 COMPANY
                                             TABLE 2
                                  STATUS OF FGD SYSTEMS DURING
                                                                Ob/77
 POWER STATION
                                                         CURRENT MONTH
             106
            1 LIGHT CO.
l.Dt NUMBER
TEXAS POWER
SANOOW NO.V
  5<*5  MW - NEW
LIGNITE

LIMESTONE SCRUBBING
STARTUP   7/80
COMBUSTION-ENGINEERING HAS BEEN CHOSEN AS THE BOILER VENDOR FOR THIS 5<*5-
Mw UNIT,  B01LLH CONSTRUCTION IS SCHEDULED TO BEGIN IN JULY 1977.  THE
UTILITY IS CURRENTLY REQUESTING/EVALUATING BIOS FOR A LIMESTONE THROWAWAY
FGU SYSTEM,  PAKTICULATE KLMOVAL IS TO TAKE PLACE ON THE COLO-SIUE OF THE
AIR HEATER.  REHEA' PLANS CURRENTLY FAVOK BYPASS OF SOI».E PORTION OF THE
FLUE-GAS.  FGD SYSTEM CONSTRUCTION is SCHEDULED FOR JULY 1973.
I.D. NUMBER  107
TEXAS POWER AND LIGHT CO.
TWIN OAKS NO. 1
  750  MW - NE.W
LIGNITE
NOT SELECTED
NOT SELECTED
STARTUP   6/63
                                      THIS UNIT WILL BE JOINTLY -OWNED BY TPftL AND ALCOA.  A FIRM DECISION HAS
                                      NOT BEEN MADE WHETHER TO INSTALL FGD FACILITIES. THIS is PRIMARILY
                                      DUE TO THE FACT THAT SUCH A DECISION IS NOT YET REQUIRED IN THE
                                      UTILITIES PLANNING TIMETABLE.
I.D. NUMBER  106
TEXAS POWER AND LIGHT CO.
TWIN OAKS NO. 2
  750  MW • NEW
LIGNITE
NOT SELECTED
NOT SELECTED
STARTUP   9/8H
                                      THIS UNIT WILL BE JOINTLY OwNED BY TPSL AND ALCOA.  A FIRM DECISION HAS
                                      NOT BEEN MADE WHETHER TO INSTALL FGD FACILITIES. THIS is PRIMARILY
                                      DUE TO THE FACT THAT SUCH A DECISION is NOT YET REQUIRED IN THE
                                      UTILITIES PLANNING TIMETABLE.
I.D. NUMBER  109
TEXAS UTILITIES
FOREST GROVE NO.
  750  MW - NEW
LIGNITE
NOT SELECTED
NOT SELECTED
STARTUP   0/Bl
                                      TEXAS UTILITIES REPORTED THAT A NEW 750-MW LIGNITE-FIRED UNIT IS IN
                                      THE EARLY PLANNING STAliE FOR THE FOREST GROVE STATION IN ATHENS* TEXAS.
                                      START-UP is SCHEDULED FOR LATE 1951.  THE BOILER WILL BE SUPPLIED
                                      BY THE BABCOCK * WlLCOX COMPANY.
I.D. NUMBER  110
TEXAS UTILITIES CO.
MARTIN LAKE NO. i
  793  MW - NEW
COAL   1.0 PERCENT SuLFuR
RESEARCH COTTRELL
LIMESTONE SCRUBBING
STARTUP  10/77
                                      THE CONTRACT FOR THIS FGO SYSTEM WAS AWARDED TO RESEARCH.COTTRELL, THIS
                                      NEW FACILITY IS NOW UNDER CONSTRUCTION, THE FGU SYSTEM STARTUP DATE IS
                                      NOW SCHEDULED FOR OCTOBER 1977. PARTICULATE REMOVAL WILL BE EFFECTED
                                      BY A RESEARCH-COTTRELL COLD-SIDE E5>n. SULFUR DIOXIDE EMISSIONS WILL
                                      BE CONTROLLED TO COMPLY WITH NSPS,
                                                                32
                                                                                            PEDCo  ENVIRONMENTAL
                                                                                                   CINCINNATI. OHIO 45246

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 COMPANY
 POWER STATION
           TABLE 2
STATUS OF FGO SYSTEMS DURING
Ob/77
                                                         CURRENT MONTH
I.D. NUMBER  111
TEXAS UTILITIES CO.
MARTIN LAKE NO. 2
  793  MW - NEW
COAL   i.o PERCENT SULFUR
RESEARCH COTTRELL
LIMESTONE SCRUBBING
STARTUP   2/78
    THE CONTRACT FOR THIS f-l»D SYSTEM WAS AWARDED TO RESEARCH-COTTRELL. THIS
    NEW FACILITY IS NOW UNDER CONSTRUCTION. THE FGO SYSTt* STARTUP DATE IS
    NOW SCHEDULED FOR THE FIRST QUARTER OF 1978.
I.D. NUMBER  112
TEXAS UTILITIES CO.
MARTIN LAKE NO. 3
  793  MW - NEW
COAL 1.0 PERCENT SULFUR
RESEARCH COTTRELL
LIMESTONE SCRUBBING
STARTUP  12/78
    THL CONTRACT FOR THIS FGD SYSTEM HAS BEEN AWARDED TO RESEARCH-COTTRELL.
    THE BOILER IS NOW BEING ERLCTE.D. START-UP IS SCHEDULED FOH DECEMBER
    1978.
I.D. NUMBER  113
TEXAS UTILITIES co.
MARTIN LAKE NO. H
  793  MW - NEW
COAL 1.0 PERCENT SULFUR
RESEARCH COTTRELL
LIMESTONE SCRUBBING
STARTUP  11/82
    THE CONTRACT FOR THIS FGD SYSTEM HAS BEEN AWARDED TO RESEARCH-COTTRELL.
    THE BOILER IS NOW BEING ERECTED. START-UP IS SCHEDULED FOR THE FOURTH
    QUARTER OF 1962.
I.D. NUMBER  114
TEXAS UTILITIES CO.
MONTICELLO NO.3
  750  MW - NEW
LIGNITE 1.0 PERCENT SULFUR
CHEMICO
LIMESTONE SCRUBBING
STARTUP   2/78
    THIS NEW STEAM BOILER WILL FIRE LOW SULFUR (0.6 TO 1.0 PERCENT SULFUR)
    TEXAS LIGNITE. THE EMISSION CONTROL SYSTEM FOR THIS UNIT CONSISTS OF
    A HIGH EFFICIENCY ESP UPSTREAM OF LIMESTONE SPRAY TOWERS. THE CONTRACT
    FOR THIS SCRUBBING SYSTEM HAS BEEN AWARDED TO CHEMICO FOR THE INSTAL-
    LATION OF THE SPRAY TOwERS. THE ESP IS A COLD-SIDE UNIT SUPPLIED By POL-
    LUTION CONTROL-WALTHER.  DESIGN PARTICULATE AND SULFUR DIOXIDE REMOVAL
    EFUCIENCY WILL ENABLE THIS UNIT TO MEET NSPS. START-UP IS SCHEDULED
    FOK THE FIRST QUARTER OF 1978.
I.D. NUMBER  115
UNITED POWER ASSOCIATION
COAL CREEK NO. 1
  5<*5  MM . NEW
LIGNITE - 0.63 PERCENT SULFUR
COMBUSTION ENGINEERING
LIME SCRUBBING
STARTUP  11/78
    THE CONTRACT FOR THIS SCRUBBING SYSTEM HAS BEEN AWARDED TO COMBUSTION
    ENGINEERING FOR THE INSTALLATION OF LIME FGD SYSTEMS ON UNITS NOS.l AND 2
    AT THIS STATION. THE SCRUBBING SySTEM FOR EACH BOILER wILL CONSIST OF
    H SPRAY TOWER ABSORBER MODULES FOR REMOVING S02 FROM THE FLUE GAS.
    ELECTROSTATIC PRECIPITATORS WILL BE INSTALLED UPSTREAM OF EACH SCRUBBING
    SYSTEM. THE UTILITY IS PLANNING TO COMMENCE FGD CONSTRUCTION BY JULY 1.
    1977.
                                                                33
                                                                                           PEDCo  ENVIRONMENTAL
                                                                                                  CINCINNATI. OHIO 45246

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  COMPANY
                                              TABLE 2
                                   STATUS  OF FGD SYSTEMS DURING   06/77
  POWER STATION
                                                         CURRENT MONTH
 I.D,  NUMBER   116
 UNITED POWER  ASSOCIATION
 COAL  CREEK MO.  2
   51*5  MW . NEW
 LIGNITE  - 0.63  PERCENT SULFUR
 COMBUSTION ENGINEERING
 LIME  SCRUBBING
 STARTUP  11/79
 THE CONTRACT  FOR  THIS  SCRUBBING  SYSTEM  HAS  BEEN  AWARDED  TO  COMBUSTION
 ENGINEERING FOR THE  INSTALLATION OF  LIME  FGD  SYSTEMS  ON  UNITS  NOS.l  AND
 2 AT  THIS  STATION. THE  SCRUBBING SYSTEM FOR EACH BOILER  WILL CONSIST OF
 t SPRAY  TOWER  ABSORBER  MODULES FOR REMOVING S02  FROM  THE  FLUE  GAS
 ELECTROSTATIC  PRECIPITATORS  WILL BE  INSTALLED  UPSTREAM OF EACH SCRUBBING
 SYSTEM.  FULL  COMMERCIAL  START-UP DATES  FOR  UNITS 1  AND 2  ARE 11/78 AND
 11/79 RESPECTIVELY.  INITIAL  OPERATIONS  WILL COMMENCE  THE  PRECEDING
 AUGUST FOR EACH UNIT.   FGD CONSTRUCTION IS  SCHEDULED  TO  COMMENCE 0«»/78
 I.D. NUMBER  117
 UTAH POWER 8 LIGHT CO.
 EMERY NO.I
  400  MW - NEW
 COAL 0.5  PERCENT SuLFUR
 CHEMICO
 LIME SCRUBBING
 STARTUP   6/78
A CONTRACT HAS BEEN AWARDED TO THE CHEMICO  AIR POLLUTION  DIVISION  FOR
A PEBBLE LIME WET SCRUBBING SYSTEM ON  THIS  NEW UNIT.  THE  SCRUBBING
SYSTEM IS DESIGNED TO OPERATE IN AN OPEN WATER LOOP MODE  WITH AN S02
REMOVAL EFFICIENCY OF ao PEKCENT FOR LOW SULFUR UTAH  COAL. PRIMARY
PARTICuLATE CONTROL wILL BE PROVIDED BY AN  ESP yPSTREAM OF THE SCRuBBERS
THE SCRUBBER SLUDGE WILL BE STABILIZED WITH FLYASH AND DISPOSED ON THE  '
PLANT SITE.  THE A-E DESIGN FIRM >-OR THIS PROJECT is  STEARNS-KOGER.
CONSTRUCTION IS UNDERWAY ON THE FGD SYSTEM  FOR THIS UNIT.
1.0. NUMBER  118
UTAH POWER > LIGHT CO.
HUNTINGTON NO.l
  415  MW - NEW
COAL  0.5 PERCENT SuLFuR
CHEMICO
LIME SCRUBBING
STARTUP  12/77
A CONTRACT HAS BEEN AWARDED TO CHEMICO AIR POLLUTION DIVISION FOR
A LIME SCRUBBING SYSTEM ON THIS NEW UNIT. MATERIALS ARE NOW ARRIVING AT
THE PLANT SITE. SITE PREPARATION AND CONSTRUCTION IS NOW UNDERWAY. THE
STATE OF UTAH REGULATIONS REQUIRE THE BEST AVAILABLE AND MOST COST
EFFECTIVE TECHNOLOGY FOR SULFUR DIOXIDE REMOVAL. PRIMARY PARTICULATE
REMOVAL WILL BE PROVIDED BY AN ESP INSTALLED UPSTREAM OF THE WET
SCRUBBING SYSTEM. LATE DELIVERY OF EQUIPMENT HAS SLOWED CONSTRUCTION
ANU START-UP IS NOW SET FOK LATE DECEMBER 1977.
I.D. NUMBER  119
WISCONSIN POWER i LIGHT CO.
COLUMBIA NO. 2
  527  MW . NEW
COAL o.a PERCENT SULFUR
CHEMICO
LIME/ALKALINE FLYASH
STARTUP   1/80
A LETTER OF INTENT HAS BEEN ISSUED TO CHEMICO FOR A LIME/FLYflSH FGD SYS-
TEM.  IT WILL CONSIST OF TWO SPRAY MODULES WITH A HOT-SIDE ESP FOR PAR-
TICULATE REMOVAL.  A CLOSED L'OOP WATER SYSTEM IS ANTICIPATED WITH FLYASH
STABILIZATION OF THE SLUDGE.  A SLUDGE DISPOSAL POND IS TO BE LOCATED ON.
SITE.  THE SCRUBBERS ARE BEING DESIGNED TO TREAT 60 PERCENT OF THE FLUE
GAi RESULTING FROM THE COMBUSTION OF LOW SULFUR COLSTKIP COAL.  THr RE-
MAINING HO PERCENT WILL BE BYPASSED FOR REHEAT.
                                                                                           PEDCo   ENVIRONMENTAL
                                                                                                  CINCINNATI. OHIO 45246

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                       TABLE  3

SUMMARY LIST OF FGD SYSTEMS IN THE EARLY PLANNING STAGES
                                               PEDCo  ENVIRONMENTAL
                                                     CINCINNATI. OHIO 45246
                             35

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3b
                        PEDCo  ENVIRONMENTAL
                             CINCINNATI. OHIO 45246

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                                          TABLE 3
               SUMMARY LIST OF FGD SYSTEMS IN THE EARLY PLANNING STAGES
  FGD STATUS REPORT 06/77

  I.D. NUMBER AND COMPANY NAME
   UNIT NAME
                  LOCATION
START UP DATE   STATUS
REG
CLASS
    1 GENERAL PUBLIC UTILITIES
    2 GENERAL PUBLIC UTILITIES
    3 GULF POWEK COt
    14 GULF POWER CO.
    5 GULF POWER CO.
    6 KENTUCKY UTILITIES
    7 POTOMAC ELECTRIC « POWER
    6 POTOMAC ELECTRIC S POWER
    9 POWER AUTHORITY OF NEW YORK
   10 SALT RIVER PROJECT
   11 SALT RIVER PROJECT
   12 SALT RIVER PROJECT
   13 SPRINGFIELD WATER  L1GHTJPOWER
   m VIRGINIA ELECTRIC AND POWER CO
COHO NO.l
SEWARD NO.7
CKIST NO. t AND NO.
CKIST NO. 6 AND NO.
LANSING SMITH NO. 1
GHENT NO. 2
CHALK POINT NO. 4
D1CKERSON NO. 4
AKTHUR KILL
NAVAJO NO 1
NAVAJO NO 2
NAVAJO NO 3
DALLMAN NO. 3
MT. STORM
           ERIE PENNSYLVANIA                   5-87       7
           SEWARD PENNSYLVANIA                 5-81       7
5          PENSACOLA FLORIDA                   0-78       7
7          PENSACOLA FLORIDA                   0-80       7
AND NO. 2  PANAMA CITY FLORIDA                 0-80       7
           GHENT KENTUCKY                      o- o       7
           PRINCE GEORGE COUNTY MARYLAND       0-80       7
           DICKERSON MARYLAND                  5-ez       7
           STATEN ISLAND NEW YORK              9-82       7
           PAGE ARIZONA                        0-07
           PAGE ARIZONA                        0-0       7
           PAGE ARIZONA                        0-0       7
           SPKINGFIELD ILLINOIS                6-78       7
           MT. STORM WEST VIRGINIA             0-0       7
                            A
                            A
                            B
                            B
                            B
                            E
                            D
                            0
                            B
                            0
                            U
                            0
                            A
                            C
7. CONSIDERING FGO SYSTEM AS WELL AS ALTERNATIVE METHODS

A.  BOILER CONSTRUCTED SUBJECT TO FEDEKAL NSPS
B,  BOILER SUBJECT TO STATE STANDARD THAT is MORE STRINGENT THAN THE FEDERAL NSPS
C.  BOILER SUBJECT To STATE STANDARD THAT IS EQUAL TO OR LESS STRINGENT THAN NSPS
0.  OTHER
E.  REGULATORY CLASS UNKNOWN
                                                              37
                                                                                         PEDCo  ENVIRONMENTAL
                                                                                                CINCINNATI. OHIO

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38
                       PEDCo  ENVIRONMENTAL
                            CINCINNATI. OHIO 45246

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                    TABLE  «t

STATUS OF FGO SYSTEMS IN THE EARLY PLANNING STAGES
                                             PEDCo  ENVIRONMENTAL
                                                  CINCINNATI. OHIO 45246

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PEDCo  ENVIRONMENTAL
      CINCINNATI. OHIO  -452-46

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 COMPANY

 POWER STATION
                     TABLE f
STATUS OF FGD SYSTEMS IN THE EARLY PLANNING STAGES DURING  Ob/77

                                 CURRENT MONTH
1.0. NUMBER    1
GENERAL PUBLIC UTILITIES
COHO NO.l
  600  MM - NEW
COAL
NOT SELECTED
NOT SELECTED
STARTUP   5/87
              STARTUP DATE CHANGED TO 5/87 FOR BOTH BOILER AND FGO SYSTEM.  LIME, LIME-
              STONE SCRUBBING, AND COAL ULSULFUKIZATION A«E THE PRIMARY PROCESSES BEING
              CONSIDERED.  NO DECISION HAS BEEN MADE YET.
1.0. NUMBER    2
GENERAL PUBLIC UTILITIES
SEWARD NO.7
  BOO  Mb - NEW
COAL
NOT SELECTED
NOT SELECTED
STARTUP   5/8«*
              STARTUP DATE CHANGED TO b/8<4 FOR BOTH BOILER AND FGD SYSTEM.
              LIMESTONE SCRUBBING, AND COAL DESULFURIZATION ARE THE PRIMARY PROCESSES
              BEING CONSIDERED.  NO DECISION HAS BEEN MADE YET.
 I.D. NUMBER    9
 GULF POWER CO.
 CRIST NO. H AND NO*  5
  150  MW - RETROFIT

 NOT SELECTED
 NOT SELECTED
 STARTUP   0/76
              EACH UNIT IS 75 MW.
              1978.
IF SCRUBBERS ARE SELECTED THEY HILL BE REQUIRED IN
I.D. NUMBER    H
GULF POWER CO.
CRIST NO. 6  AND NO.  7
  820  MW -  RETROFIT

NOT SELECTED
NOT SELECTED
STARTUP   0/80
              UNIT 6 IS 320 MW.  UNIT 7 IS 500 MW.
I.D. NUMBER    5
GULF POWER CO.
LANSING SMITH NO. 1 AND NO.
  305  MW - RETROFIT
COAL
NOT SELECTED
NOT SELECTED
STARTUP   0/80
              UNIT NO. 1 IS 125 MW.  UNIT NO. 2 IS 180 MW.  IF SCRUBBERS ARE SELECTED.
              THEY WILL BE REOUIKLD IN 1979 AND I960 ON THE RESPECTIVE UNITS.
                                                                                           PEDCo  ENVIRONMENTAL
                                                                                                  CINCINNATI. OHIO

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 COMPANY
 POWER STATION
                     TABLE <»
STATUS OF FSO SYSTEMS IN THE EARLY PLANNING STAGES DURING

                                 CURRENT MONTH
                                                                                   06/77
1.0. NUMBER    6
KENTUCKY UTILITIES
GHENT NO. 2
  510  MW - NEW
COAL   3.0 PERCENT SULFUR
NOT SELECTED
LIME SCRUBBING
STARTUP   O/ 0
              THIS NEW COAL-FIRED POWER BOILER WAS SUPPLIED BY COMBUSTION
              ENGINEERING AND IS SCHEDULED TO COMMENCE COMMERCIAL
              OPERATIONIN J1977.  THE UTILITY ALSO HAS AN EXISTING
              510-MW COAL-FIRED UNIT INSTALLED AT THIS STATION AND IS
              PRESENTLY EVALUATING PLANS TO INSTALL A SCRUBBER ON ONE
              OF THESE TWO UMTS.
I.D. NUMBER    7
POTOMAC ELECTRIC £ POWER
CHALK POINT NO. <*
  630  MW - NEW
OIL
NOT SELECTED
NOT SELECTED
STARTUP   0/80
              AWAITING PERFORMANCE RESULTS FROM MGO UNIT ON DICKERSON NO. 3 (MONTGOMERY
              COUNTY).  UNIT WILL HAVE PEABOOY-LURGI 2-STAGE VENTURI SCRUBBERS FOR PA«-
              TICULATE CONTROL.   COMPANY MAY ELECT NOT TO INSTALL FGD SYSTEM IF USE OF
              LOW SULFUR OIL IS  CONTINUED.
I.D. NUMBER    6
POTOMAC ELECTRIC & POWER
DICKERSON NO.  t
  800  MW • NEW
COAL   2.0 PERCENT SULFUR
NOT SELECTED
NOT SELECTED
STARTUP   5/82
              THERE ARE NO FIRM PLANS FOR INSTALLATION OF FGD SYSTEM.
              BOILER IS PLANNED FOR 1982.
STARTUP DATE OF
1.0. NUMBER    9
POWER AUTHORITY OF NEW YORK
ARTHUR KILL
  700  MW - NEW
COAL - 3* SULFUR - REFUSE
NOT SELECTED
NOT SELECTED
STARTUP   9/82
              THE UTILITY IS CONSIDERING BOTH REGENERABLE AND LIMESTONE SCRUBBING
              PROCESSES. FGO TECHNOLOGY IS BEING CONSIDERED FOR A FOSSIL FUEL BURNING
              UNIT WHICH WILL EMPLOY COAL AS THE PRIMARY FUEL AND OIL AS BACKUP. REFUSE
              WILL BE PROVIDED FOR SUPPLEMENTAL FUEL SUPPLIES. THE PREFERRED PLANT SITE
              IS THE ARTHUR KILL FACILITY LOCATED ON STATEN ISLAND. THE PROJECT DESIGN
              ENGINEERING FIRM IS SARGENT AND LUNDY.
I.D. NUMBER   10
SALT RIVEK PROJECT
NjrtfftdO- no i
  750  MW - RETROFIT
COAL   0.<«5 PERCENT SULFuR
NOT SELECTED
LIME/LIMESTONE SCRUBBING
STARTUP   O/ 0
              THE UTILITY IS PRESENTLY INVESTIGATING THE USE OF LOW SULFUR COAL AND
              DESULFURIZATION PROCESSES. A DEFINITIVE DECISION WILL-BE MADE PENDING
              COMPLETION OF THE SRP/t-PA STUDY. NO SPECIFIC STARTUP DATE HAS YET BEEN
              SPECIFIED.  THE CONTRACT FOR THL ESP HAS BEEN AWARDED TO JOY/WESTERN
              PRECIPITATION DIVISION.
                                                                                            PEDCo  ENVIRONMENTAL
                                                                                                  CINCINNATI. OHIO

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 COMPANY
                                             TABLE <»
                        STATUS OF FGD SYSTEMS IN THE EARLY PLANNING STAGES DURING
                                             06/77
 POWER STATION
                   CURRENT MONTH
I.D. NUMBER   11
SALT RIVEH PROJECT
NAVAJO NO 2
  750  MW - RETROFIT
COAL   0."»5 PERCENT SULFUR
NOT SELECTED
LIME/LIMESTONE SCRUBBING
STARTUP   O/ 0
THE UTILITY IS PRESENTLY INVESTIGATING THE USE OF LOW SULFUR COAL AND
DEiULFURIZATION PROCESSES. A DEFINITIVE DECISION WILL BE lAOE PENDING
COMPLETION OF THE SRP/E.PA STUDY. NO SPECIFIC STARTUP DATE HAS YET BEEN
SPLCIFItl).  THt CONTRACT FOR THE ESP HAS BLEN AWARDED TO JOY/WESTERN
PRECIPITATION DIVISION.
I.D. NUMBER   12
SALT RIVER PROJECT
NAVAJO NO $
  750  MW - RETROFIT
COAL   0,<»5 PERCENT SULFUR
NOT SELECTED
LIME/LIMESTONE SCRUBBING
STARTUP   O/ 0
THE UTILITY IS PRESENTLY INVESTIGATING THE USE OF LOW SULFUR COAL AND
OESULFUR1ZATION PROCESSES. A DEFINITIVE DECISION WILL BE MADE PENDING
COMPLETION OF THL SHP/EPA STiJDY. NO SPECIFIC STARTUP DATE HAS YET BEEN
SPLCIFIED.  THE CONTRACT FOR THE ESP HAS BEEN AWARDED TO JOY/WESTERN
PRECIPITATION DIVISION.
 1.0. NUMBER   13
 SPRINGFIELD WATER   LIGHTSPOWER
 DALLMAN NO. 3
  190  Mw - NEW
 COAL   3.0-i».3 PERCENT  SULFUR
 NOT SELECTED
 NOT SELECTED
 STARTUP   6/78
F6U SYSTEM IS UNQEK CONSIDERATION WITH  BOTH  REGENERABLE  AND  LIMESTONE
SCRUBBING BEING CONSIDERED.  BECAUSE  OF SPACE  LIMITATIONS  A  REGENERABLE
SYSTEM  IS THE LIKELY  CHOICE.   THE COMPANY  IS ALSO  CONSIDERING COMPLIANCE
THROUGH BURNING OF LOW  SULFUR  WESTERN COAL.  BOILER START-UP  HAS  BEEN
MOVED UP TO  06/78.
I.D. NUMBER    m
VIRGINIA ELECTRIC  AND  POWER  CO
MT. STORM
 11H7  MW - RETROFIT
COAL
NOT SELECTED
NOT SELECTED
STARTUP   O/ 0
 THE UTILITY  IS PRESENTLY CONSIDERING  BOTH  DESULFURIZATION AND THE  USE OF
 LOW SULFUR COAL.  A  DESULFURIZATION  SYSTEM  WOULD  TREAT  69 PERCENT OF  THE
 FLUE GAS FROM THREE BOILERS.  CONSTRUCTION  AND  STARTUP  DATES ARE CON-
 SIoERED INDEFINITE  AT  THIS  TIME.
                                                                                            PEDCo  ENVIRONMENTAL
                                                                                                  CINCINNATI. OHIO 452.46

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<*"*
                         PEDCo  ENVIRONMENTAL.
                                CINCINNATI. OHIO

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                     TABLE  5

PERFORMANCE DESCRIPTION FOR OPERATIONAL FGD SYSTEMS
                                             PEDCo ENVIRONMENTAL
                                                  CINCINNATI. OHIO

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1*6
                       PEDCo ENVIRONMENTAL
                             CINCINNATI. OHIO 45246

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                  TABLE 5
PERFORMANCE DESCRIPTION FOR OPERATIONAL FGD SYSTEMS  06/77
 IDENTIFICATION NO.
 UTILITY NAME
 UNIT NAME
 UNIT LOCATION
 UNIT RATING
 FUEL CHARACTERISTICS
 FGD VENDOR
 PROCESS
 NEW OR RETROFIT
 START UP DATE
 FGD STATUS
 EFFICIENCY,
  PARTICULATES
 ARIZONA  PUBLIC  SERVICE
 CHOLLA NO 1
 JOSEPH CITY  ARIZONA
  115 MW
 COAL   O.HH-1 PERCENT SULFUR
 RESEARCH COTTRELL
 LIMESTONE SCRUBBING
 RETROFIT
 10/73
 OPERATIONAL

 99.7 PERCENT
  S02
 58.5 PERCENT
 WATER MAKE UP
 OPEN LOOP 1.01 GPH/nu
 SLUUGE DISPOSAL
 UNSTABILIZED SLUDGE DISPOSED IN UNLINED
 UNIT COST
S57/KU CAPITAL * 2.2 MILLS/KWH ANNUALIZED
 OPERATIONAL
  EXPERIENCE
 THE BOILER OPERATED 91.81 OF THE  TIME  IN  THE PERIOD INCLUDING  MARCH,
 APRIL, & MAY. AVERA6L OPERABILITIES OF THE  A-SIDE AND B-SIDE SCRUBBERS
 HERE 89.H AND 96.6 PERCENT,  RESPECTIVELY. AVERAGE RELIABILITIES  OF  THE
 TWO SCRUBBERS FOR THE SAME PERIOD WERE 66.<» AND 93.5 PERCENT,  RESPEC-
 TIVELY. OUTAGES HERE REQUIRED FOR MID-YEAR  CLEANING AND SOME: MINOR  REPAIR
 WORK, RESEARCH-COTTRELL PERSONNEL ARE  CURRENTLY CONDUCTING  TESTS AT THIS
 PLANT TO OBSERVE THE EFFECTS OF  FOKCED SULFITE-TO-SULFATE OXIDATION
 ON THE SCRUBBEH PROCESS.
                                                                                        PEDCo  ENVIRONMENTAL
                                                                                               CINCINNATI. OHIO 45246

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                                                      BACKGROUND INFORMATION


                                                                ON

                                                           CHOLLA NO.l

     THE CHOLLA POWER STATIONt  LOCATED NEAR. JOSEPH CITY,  ARIZONA, HAS ONE 115-MW COAL-FIRED BOILER IN SERVICE AND TWO 250-MW UNITS


UNDER CONSTRUCTION.   CHOLLA NO. 1  IS  A DRY-BOTTOM PULVERIZED-COAL-FIRED UNIT DESIGNED BY COMBUSTION ENGINEERING.  THE AVERAGE

CHARACTERISTICS OF THE COAL^BURNED DURINB THE COURSE  OF  1975 ARE*  HEAT CONTENT OF 10,150 BTU/LB* ASH CONTENT OF 13.U5 PERCENT*

SULFUR CONTENT OF 0.52 PERCENT* CHLORIDE  OF 0.0<* PERCENT  (MAX.)* AND MOISTURE CONTENT OF 1«*.77 PERCENT,


     THE FGD SYSTEM AT THE CHOLLA  PLANT WAS MANUFACTURED  BY RESEARCH-COTTRELL AND INSTALLATION WAS COMPLETED ON DECEMBER 3, 1973.

THE DESIGN COMBINED SULFUR DIOXIDE REMOVAL EFFICIENCY (FOR BOTH MODULES A AND B) IS 58.5 PERCENT.  THE SYSTEM CONSISTS OF TWO

PARALLEL TRAINS (MODULES A AND  B). EACH  TRAIN IS DESIGNED FOR 2<»0,000 ACFM THROUGHPUT AT 276 F,  AND HANDLES APPROXIMATELY 50


PERCENT OF THE BOILER'S FLUE GAS LOAD. THE A-SIDE CONSISTS OF A VARIABLE THROAT FLOODED DISC SCRUBBER (FDS) FOLLOWED BY A PACKED


TOWER (MUNTERS PACKING).  THE B-SIDE  IS SIMILAR IN DESIGN.  HOWEVER, THE TOWER IS NOT PACKED AND  LIMESTONE SLURRY IS NOT CIRCU-

LATED THROUGH IT.  EITHER ONE OR BOTH OF  THE SCRUBBERS CAN BE BYPASSED.  GAS LEAKAGE AROUND EACH  TRAIN IS ESTIMATED TO BE ABOUT


i».5 PERCENT OF THE GAS BEING TREATED.  THE TOWER PACKING, WHICH IS APPROXIMATELY 2-FEET THICK, IS CONSTRUCTED OF POLYPROPYLENE


CORRUGATED SHEETS JOINED TOGETHER  IN  CRISS-CROSS PATTERNS SIMILAR TO HONEYCOMBS.  THE TOWER DEMISTERS ARE ALSO CONSTRUCTED OF

POLYPROPYLENE, AND THE REHEATERS ARE  SHELL AND TUBE TYPE CONSISTING OF THKEE TUBE BUNDLES PER UNIT.


     LIMESTONE FOR THE FGD SYSTEM  IS  PURCHASED IN GROUND FORM SUITABLE FOR SLURRYING.  THE MAIN SOURCE OF SUPPLY IS THE SUPERIOR

CO.  LOCATED NEAR PHOENIX. ARIZONA.  THIS GRADE OF LIMESTONE IS GENERALLY KNOWN AS RED WALL LIMESTONE AND IS CONSIDERED A VERY

HIGH QUALITY GRADE.  CHEMICAL SPECIFICATIONS ARE*  MINIMUM CALCIUM OXIOE CONTENT, 52 PERCENT* MINIMUM CALCIUM CARBONATE CONTENT,


95 PERCENT* MAXIMUM MAGNESIUM OXIOE CONTENT, 2 PERCENT* MAXIMUM MAGNESIUM CARBONATE CONTENT. 0.5 PERCENT* MAXIMUM SILICA CONTENT.


1 PERCENT.

     THE PLANT HAS NO SLUDGE TREATMENT OK FIXATION SYSTEMS.  THE SLUDGE  is PUMPED TO THE FLY ASH POND ON AN  INTERMITTENT BASIS


THROUGH A COMMON PIPING SYSTEM  WITH THE FLY ASH.  NO POND WATER  IS RECYCLED TO  THE FGO SYSTEM  (SOLAR EVAPORATION POND).  A GENERAL


PROCESS FLOW DIAGRAM OF THE CHOLLA FGO SYSTEM IS PRESENTED IN APPENDIX B.
                                                                "48
                                                                                           PEDCo  ENVIRONMENTAL
                                                                                                  CINCINNATI. OHIO .45346

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CHOLLA NO. 1 (CONTINUED)
PROBLEMS AND SOLUTIONS
     DECEMBER.  1973 TO APRIL 2, 197"» - BECAUSE OF A DIFFERENCE IN THE SIZE OF THE MAIN DUCT AND REHEATER TRANSITION DUCT,  THE GAS
FLOW PRODUCED HARMONIC VIBRATION*, IN THE REHEATEK.  THE VIBRATIONS WERE PARTIALLY DAMPED BY INSTALLATION OF BAFFLES.  ONE  OF THE
REHEATER TUBE BUNDLES WAS BADLY CORRODED BY ACID THAT CONDENSED IN THE UNINSULATED DUCT UPSTREAM OF THE REHEATERS.  THE TUBE
BUNDLE WAS REPLACED. AND A BAFFLE WAS INSTALLED TO DIVERT CONDENSED ACID FROM REHEATER TUBES.  ALSO. THE DUCT UPSTREAM OF  THE
REHEATER WAS INSULATED. THE ACID CONDENSATION OCCURRED ONLY IN THE B-MOOULE WHICH CONTAINS NO INTERNAL PACKING AND THEREFORE HAS
A LOWER DEGREE OF SULFUR DIOXIDE REMOVAL (25 PERCENT).
     ANOTHER PROBLLM RESULTED BECAUSE OF SOLIDS BUILDUP IN THE FDS STUFFING GLAND BOX AND ON TOP OF THE SPRAY DOME.  ALSO, SOME
LINES PLUGGED. PARTICULARLY WHEN THE SYSTEM OPERATED AT LOW FLOW RATES.  SOLIDS SETTLED OUT IN STANDBY PUMPS, AND EXCESSIVE FAN
VIBRATIONS OCCURRED BECAUSE OF ACCUMULATION OF SCALE BUILDUP WHEN THE UNIT WAS IDLE.  TO SOLVE THESE PROBLEMS, THE PACKING GLAND
POSITION WAS REVERSED  (INSTALLED UPSIDE UOWN>. THE FAN WAS SANDBLASTED. THE PIPING WAS MODIFIED TO ELIMINATE STAGNANT POCKETS. AND
PUMPS WERE FLUSHED IMMEDIATELY AFTER REMOVAL FROM SERVICE.
     OPERATION OF THE SYSTEM THROUGHOUT 1975 AND 1976 RESULTED IN THE DEVELOPMENT OF SOME ADDITIONAL PROBLEM AREAS. INCLUDING*
SIGNIFICANT CORROSION ATTACK IN THE VESSEL WALLS OF THE FLOODED-DISC PARTICULATE SCRUBBER MODULE* ACID CORROSION IN THE B-SIDE
REHEATER HOUSING* SCALE BUILDUP IN THE PIPE OUTLET AT THE SLUDGE/FLY ASH EVAPORATION POND* PLUGGING IN THE SCRUBBER TOWER  PACKING
AND MIST ELIMINATOK* EROSION IN THE PUMPS* CORROSION IN THE BOILER EXHAUST ELBOW OF THE DUCTWORK LEADING FROM THE SCRUBBERS TO THE
STACK. ADDITIONAL INFORMATION AND DATA ON THE PERFORMANCE OF THE CHOLLA FGD SYSTEM ARE PROVIDED IN THE TABLE THAT FOLLOWS.
                                                                                           PEDCo  ENVIRONMENTAL
                                                                                                 CINCINNATI. OHIO

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                                                          FGD SYSTEM RELIABILITY
                                                             CHOLLA UNIT NO.  1
                    RELIABILITY  (X)
MONTH
JAN. 7<»
FEB. 74
MAR. 74
APR. 74
MAY 74
JUN. 74
JUL. 74
AUG. 74
SEP. 74
OCT. 74
NOV. 74
DEC. 74
JAN. 75
FEB. 75
MAR. 75
APR. 75
MAY 75
JUN. 75
MODULE A
97
100
100
66
98
100
97
97
95
83
100
100
98
96

68
48
100
MODULE
90
94
66
57
99
100
92
97
99
68
98
100
99
99

65
40
100
                                                                               COMMENTS
                                             ANNUAL  BOILER  AND  FGD  SYSTEM OVERHAUL.
                                             MODULES HERE  BOTH OFF-LINE FOR MOST OF MONTH  FOR  SCHEDULED  REPAIRS  AND  CLEANING.
                                             SUBSTANTIAL PLUGGING IN THE TOWER PACKING  (A-SIDE)  AND  MIST ELIMINATORS WAS  OBSERVED.
                                             NO OTHER MAJOR PROBLEMS WERE ENCOUNTERED DURING THE PERIOD.
JUL. 75           97             96          MODULES WERE  SHUT DOWN TO  CLEAN FLOW RESTRICTIONS IN FLOOOED-DISC REC1RCULATION
                                             LINES,
AUG. 75           95            100          MODULE  A WAS  DOWN FOR  INSPECTION ONE TIME.
                                                               50
                                                                                           PEDCo  ENVIRONMENTAL
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                                                           FGO SYSTEM RELIABILITY
                                                        CHOLLA UNIT NO.  1 (CONTINUED)
                    RELIABILITY (X)
MONTH          MODULE A       MODULE B                                          COMMENTS
SEP. 75           98             97           MINOR OUTAGE DUE TO FLOOOED-OISC LINES.
OCT. 75           6<»             55           OUTAGES RESULTED FROM SCHEDULED E8UIPMENT OVERHAULS AND RECOATING OF VESSELS.
NOV. 75          100             80           NO MAJOR OUTAGES OR PROBLEMS OCCURRED DURING THE REPORT PERIOD.   MINOR PROBLEMS
DEC. 75         100             100           ENCOUNTERED INCLUDED RECYCLE PUMP REBUILDING AND MALFUNCTIONING  OF THE B-SIDE
                                             REHEATER COIL.
JAN. 76           99             99           MODULE A OPERATED 715 HOURS DURING THE REPORT MONTH, AND MODULE  B OPERATED 65t  HOURS.
                                             MODULE A EXPERIENCED SOME MINOR VALVE AND LINE PLUGGING.  MODULE B OPERATING HOURS
                                             WERE LOWER BECAUSE OF REDUCED SYSTEM REQUIREMENTS.
FEB. 76
MAR. 76
APR. 76           99             98           THE UNIT IS CURRENTLY EXPERIENCING COATING FAILURES IN THE ELBOW OF THE SCRUBBER
                                             EXHAUST DUCT.  ALSO, THE UTILITY PERFORMED SOME MINOR REPAIRS TO THE HOUSING OF THE
                                             B-SIDE REHEATER.
MAY  76           76            100           DURING THE MONTH THE A-SIDE EXPERIENCED SOME CORROSION AND PLUGGING PROBLEMS IN THE
                                             REHEATER TUBES.  IN ADDITION TO PLUGGED FDS LINES, PACKING AND OEMISTERS,  THE  UTILITY
                                             ALSO REPORTED NORMAL  HEAVY PUMP MAINTENANCE.
JUN. 76           64             39           LOW RELIABILITY FACTORS FOR THE MONTH OF JUNE RESULTED FROM A SCHEDULED MID-YEAR
                                             SCRUBBER SHUTDOWN FOR MAINTENANCE, INSPECTION AND REPAIRS.  SOME SCALING AND CORRO-
                                             SION PROBLEMS WERE UNCOVERED IN THE SYSTEM'S RECYCLE TANKS.
                                                                bl
                                                                                           PEDCo  ENVIRONMENTAL
                                                                                                  CINCINNATI OHIO 45246

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                                                           FGD  SYSTEM  RELIABILITY
                                                        CHOLLA  UNIT  NO.  1  (CONTINUED)
                    RELIABILITY  <*)
MONTH          MODULE  A        MODULE  B                                           COMMENTS
JUL. 76          100             96           DURING  THE  JULY-AUGUST  PERIOD THE  UTILITY  REPORTED  THAT  REPAIRS  TO  THE  COATING  IN  THE
AUG. 76          100            100           ELBOW OF  THE  SCRUBBER EXHAUST DUCT WERE  COMPLETED.   A  MALFUNCTIONING  SOLENOID VALVE
                                             IN  THE  DEMISTER  WASH SYSTEM OF THE B-SIDE  TRAIN,  PREVENTING  ADEQUATE  WASHING OF
                                             THE DEMISTERt  RESULTED  IN A MINOR  SCRUBBER OUTAGE.
SEP. 76         100              100           THE BOILER  REMAINED IN  SERVICE THE ENTIRE  MONTH.  A-SIDE  SERVICE  TIME  WAS 720 HOURS.
                                             B-SIDE  SERVICE TIME WAS  676  HOURS. NO OTHER  SIGNIFICANT PROBLEMS  WERE  REPORTED.
OCT. 76           56             56           THE BOILER  WAS IN  SERVICE <»17 HQUKS DURING THE  MONTH.  A-SIDE AND  B-SIDE OPERATIONAL
                                             HOURS WERE  <»15 AND 277  RESPECTIVELY.
NOV. 76           96             96           DURING  THE  MONTH THE BOILER.A-SIDE.AND B-SIDE TRAINS WERE IN SERVICE  720. 662 AND  556
                                             HOURS,  RESPECTIVELY. TWO  MINOR FORCED SCRUBBER  OUTAGES OCCURRED  DURING  THE PERIOD
                                             DUE TO  A  REHEATER  STEAM LEAK  AND INLET GAS DAMPER ADJUSTMENTS TO BOTH THE A-SIDE
                                             AND B-SIDE  SCRUBBING TRAINS.
DEC. 76           98            100           BOILER, A-SIDE.  AND B-SIDE OPERATION HOURS FOR  THE  MONTH WERE 7<*»,  7<»2  AND H9B HOURS,
                                             RESPECTIVELY.  ONE  OUTAGE  WAS  REPORTED BECAUSE OF  AN ADDITIONAL ADJUSTMENT TO THE
                                             A-SIDE  GAS  INLET DAMPER.
                                             NOTE* THE PERFORMANCE  INDEX VALVES CONTAINED  IN THE TEXT OF  THIS TABLE  ARE BASED  UPON
                                             THE MODULES'  ACTUAL SERVICE FOR A  GIVEN  PERIOD  VERSUS THE NUMBER OF HOURS THE
                                             MODULES ARE CALLED UPON TO OPERATE FOR THE SAME PERIOD.  THE  SCRUBBERS OPERATE ON  A
                                             DEMAND-ONLY BASIS. FLUE GAS IS BY-PASSED AROUND THE MODULES  WHEN THEY A"E NOT
                                             REQUIRED  FOR SERVICE  (SEE DEFINITION OF  RELIABILITY INDEX IN DEFINITIONS APPENDIX).
                                                                52
                                                                                           PEDCo  ENVIRONMENTAL
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                                                           FGD SYSTEM RELIABILITY
                                                       CHOLLA UNIT NO. 1 (CONTINUED)
                    RELIABILITY <*»
MONTH          MODULE. A       MODULE B                                          COMMENTS
JAN. 77           72             93          SERVICE HOURS FOR JANUARY* BOILER = 7
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                  TABLE 5
PERFORMANCE DESCRIPTION FOR OPERATIONAL FGD SYSTEMS  06/77
 IDENTIFICATION NO.
 UTILITY NAME
 UNIT NAME
 UNIT LOCATION
 UNIT RATING
 FUEL CHARACTERISTICS
 FGD VENDOR
 PROCESS
 NEW OR RETROFIT
 START UP DATE
 FGD STATUS
 EFFICIENCY.
  PARTICULATES
  25
 COLUMBUS I SOUTHERN OHIO ELEC.
 CONESV1LLE NO 5
 CONESVILLE OHIO
  400 MW
 COAL  «*.5 - 4.9 PERCENT SuLFuR
 UNIVERSAL OIL PRODUCTS
 LIME SCRUBBING
 NEW
  2/77
 OPERATIONAL

 99.6 PERCENT
  S02
 89.5 PERCENT
 WATER MAKE UP
 SLUUGE DISPOSAL
  STABILIZEU SLUDGE DISPOSED IN  UNLINED PONQ
 UNIT COST
*15.27 MILLION CAPITAL * 5.6! MILLS/KWH OPERATING
 OPERATIONAL
  EXPERIENCE
 REFER TO THE BACKGROUND INFORMATION SECTION IN TABLE 5 OF THIS REPORT.
 THE BOILER AND ESP WERE COMPLETED AND PLACED IN SERVICE IN SEPT. 1976.
 THE B-SIDE MODULE BECAME AVAILABLE FOR SERVICE IN JANUARY 1977.
 COMMERCIAL OPEKATIONS WERE ACHIEVED ON FEBRUARY 13. 1977. THE EMISSION
 CONTROL SYSTEM FOR THIS UNIT CONSISTS OF A COLU-SIDE ESP FOLLOWED BY
 TWO TCA LIME SCRUBBING MODULES SUPPLIED BY UOP. DRAVO IS SUPPLYING THE
 TH10SOHBIC LlML SCKUBBlNG REAGENT. IUCS IS SUPPLYING THEIR POZ-0-T£C
 SLUDGE STABILIZATION FACILITY. B-SIDE STARTUP IS SCHEDULED FOR JAN. 1978.
                                                                                        PEDCo  ENVIRONMENTAL
                                                                                               CINCINNATI. OHIO  45246

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                                                      BACKGROUND INFORMATION


                                                                ON


                                                         CONESVILLE NO. 5


     THE CONESVILLE POWER STATlOf. IS LOCATED ON THE MUSKINGUM RjVEK, APPROXIMATELY 7«»0 FEET ABOVE SEALEVELt NEAR COSHOCTON, IN


NORTHEAST OHIO.  THE PLANT HAS A CURRENT CAPACITY OF 16
-------
CONESVILLE NO. 5 (CONTINUED)
OP 90 TO 95 PERCENT.   THE LINE SLAKER DISCHARGED THE 20 PERCENT  SOLIDS SLURRY INTO AN AGITATED LIME SLURRY SUMP WHERE IT IS RE-
TAINED FOR A 5-MINUTE PERIOD  PRIOR TO TRANSFER TO THE LIME SLURRY  STORAGE TANK,  WHICH HANDLES THE SURGE REQUIREMENTS OF THE AB-
SORPTION SYSTEM.  THE TRANSFER OF SLURRY  FROM THE STORAGE TANK  TO  THE TCA RECYCLE TANKS IS ACCOMPLISHED 8Y VARIABLE SPEED PUMPS
WHICH RESPOND TO CHANGING S02 AND LOAD CONDITIONS VIA A PH MONITOR.   THE SCRUBBING LIQUOR CONTAINS ABOUT 7 TO 12 PERCENT SOLIDS.
THE ABSORBENT LIOUOR  IS RECIRCULATED  BY t PUMPS (1 STANDBY)  EACH RATED AT 12.000 GPM.  SCRUBBER OUTLET PH IS 5.8,  AND PH IN THE
RECYCLE TANK IS APPROXIMATELY 6.6.
     A BLEED STREAM OF SPENT  REACTION PRODUCTS IS CONTINUOUSLY  WITHDRAWN FROM THE TANK PUMPED TO THE THICKENER SYSTEM.  THE
THICKENER IS 100 FT IN DIAMETER AND 1<* FT DEEP IN THE CENTER.   HERE  THE REACTION PRODUCT SLURRY IS CONCENTRATED TO AN UNDERFLOW
COMPOSITION OF APPROXIMATELY  <»0 PERCENT SOLIDS.  THIS UNDERFLOW  IS CYCLED TO THE IUCS FIXATION FACILITIES WHERE IT IS FURTHER
THICKENED, VACUUM FILTERED AND MIXED  WITH A BLEND OF DRY FLY ASH AND LIME TO FORM A 73 PERCENT SOLIDS SUBSTANCE (IUCS P02-0-TEC).
THE PRODUCT IS BEING  CYCLED TO A 3500 ACRE-FOOT DIKED POND,  SCHEDULED TO BE ADEQUATE FOR 5 YEARS OF OPERATIONS.
     THE WASTE WATER  POND, WHICH WILL RECEIVE THE ASH WATER. COOLING WATER BLOWNDOWN AND WATER FROM THE SLUDGE TREATMENT PLANT
IS EXPECTED TO OVERFLOW INTO  THE MUSKlNGUM RlVER DURING LOW LOAD PERIODS AND CANNOT,  THEREFORE DURING THESE PERIODS, THE SYSTEM
WILL NOT BE CLOSED LOOP.  HOWEVER, AT HIGH LOAD PERIODS, THE INCREASED DEMAND FOR POND WATER IS EXPECTED TO RENDER THE SYSTEM
CLOSED LOOP.
     REFER TO APPENDIX B FOR  A GENERAL PROCESS FLOW DIAGRAM.
                                                                56
                                                                                           PEDCo  ENVIRONMENTAL
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MONTH/YR
DEC. 76
   MODULE
AVAILABILITY
 (PEHCLNT)
A       B
   MODULE
OPERABILITY
 (PERCcM)
 A       B
 JAN.  77
 FEB.  77
       OPERATING HISTORY

        CONESVILLE NO. 5




                            COMMENTS

soz REMOVAL OPERATIONS WERE SCHEDULED TO COMMENCE IN DECEMBER.

HOWEVER A MAJOR FIRE IN MODULE N0.5A DELAYED START-UP.

THE FIRE CAUSED $2.1 MILLION DAMAGE TO THE MODULE.  THE UTILITY'S

INSURANCE COVERED THE DAMAGE AND A NEW SCRUBBER MODULE WILL BE

PURCHASED FROM AND INSTALLED BY U.O.P.  THE 5A MODULE IS SCHEDULED

TO COMMENCE OPERATIONS  IN JULY 1977.

THE UTILITY IS CURRENTLY OPERATING AIR AND WATER TESTS ON MODULE SB

AND SCRUBBING OPERATIONS WITH SB ARE NOW SCHEDULED FOR JANUARY.

INITIAL  START-UP FOR  DEBUGGING AND COMMISSIONING PURPOSES OCCURRED

IN EARLY JANUARY.  EARLY OPERATIONS WERE MARKED BY COLO WEATHER-RELATED

PROBLEMS SUCH AS FROZEN LINES AND GEARSt CRACKED FLANGES. A FROZEN

LIME  BELT CONVEYER. AND A FROZEN PIPELINE FROM THE THICKENER  TO THE

IUCS  FACILITY.  COMMEKClAL  AVAILABILITY FOR SERVICE OCCURRED  ON JAN-

UARY  27.  NO JANUARY  OPERATING HOURS ARE AVAILABLE.

COMMERCIAL START-UP OF  MODULE SB ACHIEVED ON FEBRUARY 13. 1977.

AFTER  START-UP, THE SCRUBBER LOGGED 286 HOURS OF OPERATION.   THE

LONGEST PERIOD OF CONTINUOUS OPERATION WAS 132 HOURS.  THE BOILER LOG-

GED 668 HOURS DURING  FEBRUARY.  PROBLEMS INCLUDED PRESSURE SURGES

IN THE PRESATURATOR PIPING  LINE. UNSATISFACTORY OPERATION OF  THE

CONTINUOUS S02 ANALYZERS. POOR VELOCITY DISTRIBUTION THROUGH  THE TCA

BEDS.  AND CARRYOVER OF  SCRUBBING LIQUID INTO THE MIST ELIMINATOR SECTION.

THE ESP IS REPORTED TO  BE OPERATING SATISFACTORILY.  COMPLIANCE TESTING

FOR THIS UNIT IS SCHEDULED  FOR MAY 1977.
                                                                                            PEDCo  ENVIRONMENTAL
                                                                                                   CINCINNATI. OHIO 45246

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CONESVILLE NO.  5 (CONTINUED)
           OPERATION TIME (HR)
PERIOD   BOILER    fl-SIDE    B-SIDE
APR. 77    685                  261
AVAILABILITY =  <»2 PERCENT
OPERABILITY = 38 PERCENT
RELIABILITY = i»0 PERCENT
UTILIZATION r 37 PERCENT
HAY  77    712                  355
AVAILABILITY =  58 PERCENT
OPERABILITY = 50 PERCENT
RELIABILITY = 51 PERCENT
UTILIZATION = 50 PERCENT
                                        COMMENTS
THE UTILITY REPORTED A NUMBER OF PROBLEM AREAS REGARDING SCRUBBER OPERATIONS
DURING THE REPORT PERIOD. SPECIFICALLY. SOME CORROSION HAS BEEN REPORTED IN THE
PRESATURATOR AREA <3l6 SS CONSTRUCTION!, THE RUBBER LINER IN THE RECYCLE TANK IS
PEELING OFF (PROBABLY AN APPLICATION PROBLEM), SOME PLUGGING IN THE TUBE
THICKENERS HAS OCCURRED, AND THE QUALITY OF THE LIME SUPPLY HAS BEEN A REAL
PROBLEM AREA (ROCKS UP TO FIVE INCHES IN DIAMETER HAVE BEEN DETECTED!. THE
LATTER ITEM HAS PROMPTED DRftVO TO INSTALL MECHANICAL SEPARATORS AND METAL
DETECTORS AT THE LIME SHIPMENT FACILITY. A STACK OUTLET TEMPERATURE OF 200F IS
BEING MAINTAINED IN ORDER TO MINIMIZE ACID RAINOUT AND STACK CORROSION PROBLEMS.
                                                                56
                                                                                           PEDCo  ENVIRONMENTAL
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                  TABLE 5
PERFORMANCE DESCRIPTION FOR OPERATIONAL FGD SYSTEMS  06/77
 IDENTIFICATION NO.
 UTILITY NAME
 UNIT NAME
 UNIT LOCATION
 UNIT RATING
 FUEL CHARACTERISTICS
 FGO VENDOR
 PROCESS
 NEW OR RETROFIT
 START  UP DATE
 FGD STATUS
 EFFIClENCYt
   PARTICULARS
 SO
COMMONWEALTH EDISON
HILL COUNTY NO 1
ROMEOVILLE ILLINOIS
 167 HW
COAL "».0  PERCENT  SULFUR
BABCOCK ft WILCOX
LIMESTONE SCRUBBING
RETROFIT
  2/72
OPERATIONAL

98 PERCENT
   S02
 62 PERCENT
  WATER MAKE UP
 OPEN LOOP 1.66 GPM/MW
  SLUDGE DISPOSAL
  UNIT COST
  OPERATIONAL
   EXPERIENCE
  STABILIZED SLUDGE DISPOSED IN  HAULAWAY TO LANDFILL
S113/KW CAPITAL * 13 MILLS PER KUH OPERATING
 REFER TO THE BACKGROUND INFORMATION SECTION IN TABLE 5 OF THIS REPORT.
 THIS FULL SCALE DEMONSTRATION SCRUBBING SYSTEM HAS BEEN IN SERVICE SINCE
 FEBRUARY 1972. THE FGD SYSTEM INCLUDES TWO SCRUBBING TRAINS FOR THE
 CONTROL OF PARTItULATES ANU SULFUR DIOXIDE. MODULE AVAILABILITY,
 OPERABILITY, RELIABILITY.  AND UTILIZATION INDEX VALUES FOR THE REPORT
 PERIOD ARE PROVIDED IN TABLE 5.  A SLUDGE. STUDY, CONDUCTED BY UOP,  AND A
 MAGNESIUM INNOCULATION AND FORCED OXIDATION STUDY, CONDUCTED BY THE
 UTILITY, WERE COMPLETED DURING THE REPORT PERIOD.
                                                                                         PEDCo  ENVIRONMENTAL
                                                                                               CINCINNATI. OHIO  45246

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                                                     BACKGROUND INFORMATION
                                                              ON
                                                       WILL COUNTY NO. 1
     IN 1970. COMMONWEALTH EDISON CONTRACTED WITH THE BECHTEL CORPORATION TO INVESTIGATE THE SULFUR REMOVAL SYSTEMS THEN AVAILABLE
HAVING A SUFFICIENT DEGREE OF DEVELOPMENT TO WARRANT LARGE-SCALE INSTALLATION! ON WILL COUNTY STATION'S UNIT NO. i.  AFTER DECIDING
ON A WET SCRUBBER SYSTEM USING LIME OR LIMESTONE. BECHTEL PREPARED A SPECIFICATION AND RELEASED IT FOR BID. FROM NINE BIDDERS THAT
WERE SOLICITED, SEVEN PROPOSALS WERE RECEIVED.  AFTER DETAILED STUDY A'MD BlO EVALUATION WITH SPECIAL CONSIDERATION OF THE PROJECT
SCHEDULE, BABCOCK AND WILCOX WAS AUTHORIZED IN SEPTEMBER 1970 TO BEGIN DETAILED ENGINEERING FOR A LIMESTONE SLURRY SYSTEM.  COM.
PLETION DEADLINE FOR THE PROJECT WAS DECEMBER 31, 1971, A DEADLINE ESTABLISHED BY THE ILLINOIS COMMERCE COMMISSION AS PART OF A
RATE CASE.
     THE BABCOCK AND WILCOX PROCESS WAS GUARANTEED To REMOVE 98 PERCENT QF THE FLY ASH AND 76 PERCENT OF THE SULFUR DIOXIDE. THESE
EFFICIENCIES WERE BASED ON A DUST INLET LOADING OF 1.355 GRAINS PER STANDARD CUBIC FOOT AT 70 F AND ON BURNING OF ILLINOIS COAL
CONTAINING 
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WILL COUNTY (CONTINUED)

SLUDGE FROM THE SYSTEM IS SENT TO A CLARIFIER.  THE OVERFLOW IS HETURNED TO THE PROCESS AND THE UNDERFLOW IS STABILIZED BY MIXING

IT WITH LIME AND FLY ASH.  APPROXIMATELY 200 POUNDS OF LIME AND tOO POUNDS OF FLY ASH ARE USED PER TON OF DRY SOLIDS OF SLUDGE.

THE SLUDGE IS STABILIZED IN AND TRANSPORTED BY CONCRETE MIXING TRUCKS FOR ULTIMATE DISPOSAL IN AN OFF-SITE DISPOSAL

AREA.

PROBLEMS AND SOLUTIONS

     1972 - DEHISTER PLUGGING WAS A CONSTANT PROBLEM, MAINLY BECAUSE OF HEAVY LIMESTONE ACCUMULATION ON THE BOTTOM OF THE DEMISTER

AND ALSO BECAUSE OF LOW WASH-WATER PRESSURE CAUSED BY LEAKS IN THE POND RETURN BYPASS.  BECAUSE OF THESE PROBLEMS, MODULES A AND B

WERE OUT OF SERVICE FOR SEVERAL DAYS EACH MONTH DURING MARCH, APRIL, JUNE, AND JULY 1972.  THE MODULES WERE ALSO OUT OF SERVICE

FROM SEPTEMBER 26 TO NOVEMBER 21' 1972* BECAUSE THE BOILER WAS DOWN.

     IN ORDER TO SOLVE THE DEMISTER PROBLEM, THE SLURRY NOZZLES WERE LOWERED AND  THE SLURRY CIRCULATION SYSTEM WAS LEFT OUT OF

SERVICE TO KEEP THE DEMISTER CLEAN.  SINCE  THE SITUATION DID NOT  IMPROVE,  THE DEMISTER ELEMENTS WERE HAND-WASHED.  THIS SOLVED THE

PROBLEM PARTIALLT, BUT CAUSED DIFFICULTY WITH THE  VENTURI  NOZZLES BECAUSE  BROKEN  ELEMENTS FROM THE DEMISTER GOT  INTO THE SLURRY

SYSTEM.

     AT HIGH GAS FLOW RATES, THE  REHEATER OF MODULE B  VIBRATED EXCESSIVELY.  THEREFORE, MODULE B  WAS TAKEN OUT OF SERVICE IN APRIL

TO ALLOW  REHEATER MODIFICATIONS,  WHICH  INCLUDED REBRACING  OF THE  REHEATER  TUBES AND INSTALLATION  OF A BAFFLE PLATE TO REDUCE THE

VIBRATIONS.

     OTHER  REASONS FOR OUTAGES  WERE EROSION AND PLUGGING OF SPRAY NOZZLES, INTERNAL AND EXTERNAL  BUILDUP OF DEPOSITS ON VENTURI

NOZZLES,  CORROSION, SULFITE BLINDING PROBLEMS, AND FAN VIBRATIONS.

     1973 - DEMISTER  PLUGGING CONTINUED.  FURTHERMORE, THE DEMISTER ON MODULE B BROKE LOOSE FROM  ITS MOUNTINGS AND THE RESULTANT

CARRYOVER OF WASHWATER PLUGGED  THE REHEATER.  THIS REHEATER ALSO  LEAKED BECAUSE OF CHLORIDE PITTING CORROSION.   MODULE A WAS DOWN

FROM APRIL  21* TO MAY  2H«  1973,  AND MODULE B REMAINED OUT OF SERVICE FROM MAY 1973 TO MAY 20,  1975.  THERE WAS NO SCRUBBER OPERA

TION FROM AUGUST 27 TO SEPTEMBER  26. 1973.

     IN EFFORTS TO SOLVE  THE DEMISTER AND REHEATER PROBLEMS,A CONSTANT UNOERSPRAY AND INTERMITTENT OVERSPRAY WERE USED TO WASH ALL

THE DEMISTER COMPARTMENTS OF MODULE A.  EXTRA NOZZLES WERE ADDED  AND A CLEAN WATER SUPPLY WAS MAINTAINED.  THE REHEATER UNIT UAS

ALSO RETUBED.

     197i» - ONLY MODULE A OPERATED DURING 197<». THE MAIN PROBLEMS  WERE FREEZING OF THE VENTURI THROAT DRIVE MECHANISM, TANK SCREEN

BLINDING,  DUCT CORROSION, AND VIBRATIONS,   LOSS OF BUILDING HEAT  CAUSED EXTENSIVE DAMAGE AND KEPT THE SYSTEM DOWN FOR THE ENTIRE

                                                                61

                                                                                                         ENVIRONMENTAL.
                                                                                                  CINCINNATI. OHIO 45246

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HILL COUNTY (CONTINUED)

MONTH OF JANUARY 197<».

     1975 - ENTERING 1975 MODULE A WAS OPERATIONAL AND MODULE B WAS STILL UNDERGOING MODIFICATION.  IN THE FIRST QUARTER OF 1975

THERE WERE 6 A-MODULE OUTAGESt ONE OF WHICH WAS A FORCED OUTAGE. DUE TO THE SPLITTING OF A SLURRY VENTURI SUPPLY HOSE.  MODULE 6

WAS RETURNED TO SERVICE ON MAY 20. 1975.   THE UTILITY DECIDED TO OPERATE THE SCRUBBER ON ILLINOIS HIGH-SULFUR COAL.  WHEN THIS

OPERATION BEGAN. A MULTITUDE OF PROBLEMS  OCCURRED*  LOwER PARTICULATE REMOVAL EFFICIENCIES. HIGH SLURRY CARRYOVERS. DEMISTER

PLUGGING, REHEATER COIL FOULING AND LEAKS.   MODULE A WAS TAKEN OUT OF SERVICE IN MID-JUNE FOR THE REMAINDER OF 1975.  BY MID.

SEPTEMBER 1975 MODULE B WAS TAKEN OUT OF  SERVICE OWING TO MASSIVE SCALING IN THE ABSORBER SYSTEM.  FINALLY, UNIT NO. 1 WAS SHUT

DOWN FOR OVERHAUL OF THE BOILER. TURBINE. AND SCRUBBER IN MID-OCTOBER* THIS OUTAGE LASTED MORE THAN 
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PERIOD             OPERABILITY («)
MONTH/YEAR       MODULE A   MODULE B
MAR. 72
APR. 72
 MAT  72
 JUN.  72
 JUL.  72
 AUG.  72
 SEP.  72
OCT. 72
                               35
70
32
          31
79
21
          30
         FGD SYSTEM OPERABILITY
         WILL COUNTY UNIT NO. 1
                        COMMENTS
MODULE A DOWN FOR REPAIR AND MODIFICATION OF OEMISTER WASH PIPING ASSEMBLY.
MODULE B WAS REMOVED  FROM SERVICE EVERY 2 OR 3 DAYS TO HAND-WASH THE DEMISTER. OTHEK
PROBLEMS WERE VIBRATION OF REHEATER TUBE BUNDLL, RAPID EROSION OF SCRUBBER SPRAY
NOZZLES. PLUGGING OF VENTURI NOZZLES.
MODULE A OUT OF SERVICE FUR 6 DAYS BECAUSE OF NEAR-RUPTURE OF A VENTURI PIPE
EXPANSION JOINT & HEAVY BUILDUP OF SOLIDS ON DEMISTER.  MODULE B OUT OF SERVICE MOST
OF THE TIME FOR SIMILAR REPAIR OF VENTURI PIPE  EXPANSION JOINT, AND FOR MODIFICATION
OF REHEATER UNIT AND DEMISTER WASH SYSTEM.
A TWO.WEEK OUTAGE OF MODULE B WAS INCURRED TO REBRACE THE REHEATER UNIT. INSTALL
UNDERSPRAY NOZZLES ON  DEMISTER. AND  INSTALL HEAVIER  SCREENS  IN THE SUMP.   REHEATER
PLUGGING CAUSED .ADDITIONAL OUTAGES.
BOTH  MODULES WERE OUT  OF  SERVICE OWING  TO HIGH  DIFFERENTIAL  PRESSURE ACROSS THE
DEMISTERS. LEAKAGE OF  A POND RETURN  BYPASS VALVE  CAUSED DEMISTER PLUGGING.  ALSO
DURING THIS PERIOD. THE RUBBER LINING IN MODULE A  .

PLUGGING OF VENTURI NOZZLES AND DEMISTER CAUSED SHUTDOWN OF  MODULE A FOR 2 DAYS FOR
REPAIRS.  MODULE B WAS OUT OF SERVICE FOR 22 DAYS  FOR CLEANING OF THE DEMISTER AND
REHEATER UNIT, INSTALLATION OF OVERHEAD SPRAY NOZZLES, AND REPLACEMENT OF  SECTIONS OF
THE DEMISTER.  THE UNIT WAS SHUT DOWN FOR TWO DAYS FOR TURBINE-GENERATOR REPAIR.
BOILER DOWN SEPT. 1-5  BECAUSE OF NO  DEMAND.  I.D.  FAN PROBLEM CAUSED UNSTABLE OPERA-
TION  OF THE BOILER MOST OF THE MONTH.  MODULE A WAS  DOWN FOR MODIFICATION  OF REHEATER
UNIT  AND REPAIR OF RECIRCULATION TANK SCREENS.
BOILER AND SCRUBBERS WERE DOWN.  PRINCIPAL MODIFICATIONS INCLUDED INSTALLATION OF
REHEATER BAFFLE PLATES TO DAMPEN VIBRATIONS AND INSTALLATION OF AN EXPERIMENTAL
                                                                                           PEDCo  ENVIRONMENTAL
                                                                                                  CINCINNATI. OHIO  452-ae

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 PERIOD
 MONTH/YEAR
 NOV.  72
 DEC.  72

 JAN.  73
 FEB.  73

 MAR.  73

 APR.  73
  OPERABILITY  (*)
MODULE A   MODULE  B
OCT. 73
NOV. 73
DEC. 73
     0
    22


     0
    22

    65
                     32
                     51
 0
30
11
              13
MAY
JUN.
JUL.
AUG.
SEP.
73
73
73
73
73
0
16
51
19
0
0
0
0
0
0
   WILL COUNTY UNIT NO. 1 (CONTINUED)
                        COMMENTS
DEMISTER WASH SYSTEM.
BOILER PROBLEMS CAUSING UNSTABLE OPERATION KEPT BOTH MODULES DOWN DURING THIS MONTH.
MODULES OPERATED INTERMITTENTLY BECAUSE OF ELECTROSTATIC PRECIPITATOR TESTING AND
MISCELLANEOUS INSTRUMENT PROBLEMS.
BOTH MODULES WERE DOWN FOR REPAIRS AND MODIFICATIONS.
MODULES WERE OUT OF SERVICE BECAUSE OF CRACKS IN THE INLET DUCTWORK OF THE BOOSTER
FAN.  IMPROPER INSTALLATION OF THE Qt-MISTER IN THE B-SIDE CAUSED REHEATER PLUGGING.
MODULE A WAS OUT OF SERVICE FOR 5 DAYS BECAUSE OF DEMISTER PLUGGING.  BOILER WAS DOWN
FOR n DAYS OF INSPECTION.  MODULE B WAS DOWN BECAUSE OF LEAKS FROM REHEATER TUBES.
PERSISTING PROBLEMS WITH DEMISTER AND DEPOSITS OF CALCIUM SULFATE SCALE ON REHEATER
TUBES OF MODULE A WERE ENCOUNTERED DURING THE MONTH.
BOTH MODULES WERE OUT OF SERVICE DURING THIS MONTH.
MODULE B WAS KEPT DOWN TO ALLOW CONCENTRATION ON THE PROBLEMS WITH MODULE A.  BOILER-
RELATED PROBLEMS WERE RESPONSIBLE FOR MOST OF THE OUTAGES OF MODULE A.
MODULE A PROBLEMS*  REHEATER TUBES LEAKS AND HIGH FAN VIBRATIONS.
MORE REHEATER TUBE LEAKS ON MODULE A ATTRIBUTED TO CHLORIDE CORROSION ATTACK.
MODULES WERE DOWN.  DURING THIS MONTH, CHICAGO FLY ASH CO. FINISHED CLEANING AND
TREATING THE NORTHEAST HALF OF THE SLUDGE POND.
MODULE A TRIPPED SEVERAL TIMES BECAUSE OF BAD LIMIT SWITCHES IN THE BYPASS AND BLOCK
DAMPERS.  UNIT WAS ALSO TAKEN DOwN TO BALANCE THE BOOSTER I.D. FAN.
ROUTINE INSPECTION OF MODULE A REVEALED SOME PLUGGING,  MODULE WAS KEPT DOWN FOR
CLEANING AND SOME MODIFICATION.  POOR GAS DISTRIBUTION IN MODULE SUSPECTED TO CONTRI-
BUTE TO DEMISTER PROBLEMS.
MODULES WERE DOWN.  THE MONTH WAS DEVOTED TO MODIFICATION AND MAINTENANCEi MOSTLY OF
                                                                £.<*
                                                                                            PEDCo  ENVIRONMENTAL
                                                                                                   CINCINNATI. OHIO  45246

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                                                HILL COUNTY UNIT NO. 1 (CONTINUED)
 PERIOD
MONTH/YEAR
JAN. 74
FEB. 7*
MAR. 7*
APR. 74
MAY  74
JUN. 74
JUL. 74
AUG. 74
SEP. 74
OCT. 74
  OPERABILITY (k)
MODULE A   MODULE B
    21
    72
     93
     55
     96
     91
     85
    94
                                       COMMENTS
OEMISTERt VENTURI THROATSt PUMPS. AND ISOLATION VALVES.
MODULES WERE DOWN OWING TO FREEZING IN THE 10-lNCH-OlAMETEH,  4400-FT. LINE BETWEEN
MODULES AND POND.  SOME DAMAGE TO SUMP PUMPS.  FREEZING ALSO DAMAGED SOME INSTRUMENTS
THE FROZEN PIPELINE WAS THAWED. REANCHORED. AND RETURNED TO SERVICE.  THE INSTRUMENTS
DAMAGED BY FREEZING WERE REPAIRED.  MODULE A KEPT DOWN UNTIL ARRIVAL OF SECOND-STAGE
OEMISTER.
MODULE A WAS READY FOR SERVICE MARCH 20 BUT WAS NOT RETURNED TO SERVICE TILL MARCH 27
BECAUSE BOILER WAS DOWN.
MODULE A CONTINUED TO OPERATE UNTIL APRIL 19CEXCEPT FOR TWO SHORT INSPECTION OUTAGES)
FOR 23 CONSECUTIVE DAYS.  OPERATION WAS ON LOw-SULFUR COAL. SUMP SCREEN FROM MODULE B
WAS SUBSTITUTED  FOR DAMAGED SCREEN IN MODULE A.
MODULE A OPERATED FOK ENTIRE MONTH EXCEPT FOR SHORT OUTAGES FOR INSPECTION.  MUCH OF
THIS OPERATION WAS ON HIGH-SULFUR COAL.
MODULE A OPERATED FOR ABOUT 300 HOURS.  THE SYSTEM WAS OFF FOR 2 WEEKS FOR REPAIR OF
VENTURI THROAT DRIVE
MODULE A OPERATED FOR THE ENTIRE MONTH EXCEPT FOR ONE INSPECTION OUTAGE AND TWO
BOILER SHUTDOWNS.  MODULE B REMAINS DOWN UNTIL SATISFACTORY OPERATION OF MODULE A IS
ACHIEVED.
MODULE A WAS DOWN SIX TIMES THIS MONTH* THREE TIMES BECAUSE OF NO BOILER DEMAND,
TWICE FOR REPAIR OF LEAKS IN STEAM PIPING, AND ONCE FQR BALANCING OF A FAN.
MODULE A WAS OFF THREE TIMES*  ONCE FOR CLEANING OF DEPOSITS FROM THE VENTURI THROAT,
ONCE FOR REPAIR OF A DESUPERHEATER LEAK. AND ONCE BECAUSE BOILER WAS DOWN.
MODULE A WAS DOWN FOUR TIMES*  ONCE BECAUSE OF BOILER OUTAGES, ONCE FOR INSPECTION,
AND TWICE FOR REPAIR OF HEHEATER LEAKS.
                                                                                         PEDCo  ENVIRONMENTAL
                                                                                                CINCINNATI. OHIO  45246

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 PERIOD
MONTH/YEAR
NOV. 7"»
DEC.
JAN. 75
FEB. 75
  OPERABILITY <*)
MODULE A   MODULE  B
    97        0
                     99
                    99
   WILL COUNTY UNIT NO. 1 (CONTINUED)
                                       COMMENTS
MODULE A WAS OUT OP SERVICE. THREE TIMES* TWICL BECAUSE OF NO DEMAND AND ONCE FOR
INSPECTION.
MODULE A WAS DOWN TWICE*  ONCE FOR INSPECTION AND ONCE FOR REPAIR OF VALVE IN SPENT.
LIOUOR LINE TO POND.
MODULE A WAS DOWN TWICE*  ONCE FOR INSPECTION AND ONCE FOR NO DEMAND.  MODIFICATION
OF MODULE B IS CONTINUING.
MODULE A WAS OUT OF SERVICE TWICE*  ONCE FOR INSPECTION AND ONCE FOR NO DEMAND.  ONE
SMALL REHEATER LEAK IN A STAINLESS STEEL BUNDLE WAS BLANKED-OFF ON-LINE.  DURING THE
INSPECTION, DEMISTER UNDERWASH NOZZLES WERE CLEANED AND A SMALL SECTION OF DEMISTER
WAS REPLACED.  INSPECTION SHOWED THAT CONDITIONS INSIDE THE SCRUBBER WERE ABOUT THE
SAME AS BEFORE.  COAL  BURNED THIS MONTH AVERAGED LESS THAN i« SULFUR. MODIFICATION OF
MODULE B IS CONTINUING.  CHICAGO FLT ASH IS TREATING MATERIAL FROM  THE SCRUBBER WITH
PORTLAND CEMENT AND FLY ASH AND DUMPING THE TREATED MATERIAL INTO THE NORTH  HALF OF
THE HOLDING BASIN.
                                                                                            PEDCo  ENVIRONMENTAL
                                                                                                   CINCINNATI. OHIO  45246

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                                                WILL COUNTr UNIT MO. 1 (CONTINUED)
 PERIOD    MODULE
MONTH/YEAR
MAR. 75        A
           SYSTEM PERFORMANCE FACTORS (ft)
       AVAILABILITY  OPERABILITY  RELIABILITY  UTILIZATION
                          99
                                                      93
APR. 75
            37
                          35
MAY  75
A

B
                           84

                           37
84

37
84

37
84

37
                        COMMENTS
MODULE A WAS DOWN FOUR TIMES* TWICE FOR NO DEMAND,
ONCE FOR A VENTURI HOSE LEAK, ONCE FOR AN ACCIDEN-
TAL 50-MINUTE TRIP.  THE SYSTEM OPERATED ON LOW
MODULE B SULFUR COAL DURING THE MONTH.  MODIFICATI
ARE CONTINUING.
SLUDGE PONU WAS OVERBURDENED BY NEAR-CONTINUOUS
OPERATION OF MODULE A.  THE FGD SYSTEM WAS SHUT
DOWN TO ALLOW EVAPORATION OF WATER FROM THE POND.
DURING SHUT DOWN, THE FOLLOWING MODIFICATIONS WERE
HADE*  PUMP GLAND WATER FLOWS WERE REDUCED FROM 10
TO b GPM*FILTER BACKWASH WAS ROUTED OUT OF SYSTEM*
CONTINUOUS DEMISTER UNDERSPRAY WAS CHANGED TO
INTERMITTENT.  RECLAIM COAL WAS BURNED IN THE
BOILER DURING THE MONTH.
MODULE A REMAINED OUT OF SERVICE UNTIL MAY 5, WHEN
IT WAS DETERMINED THAT THERE WAS ENOUGH FREEBOARU
IN THE POND To START OPERATING.  THERE WERE TWO
MORE OUTAGES*  ONE FOR 45 HINUTES, THE RESULT OF A
DAMPER TRIP* THE OTHER FOR CLEANING OF UNOERSPRAY
NOZZLES.  MODULE B WAS PLACED IN SERVICE AT TEN
A.M., MAY 20, FOR THE FIRST TIME SINCE NOON ON
APRIL 13, 1973.  AFTER BRIEF STARTUP, WHICH WAS
ROUTINE, OPERATION WAS DELAYED UNTIL THE 20TH
BECAUSE OF TWO BROKEN OIL PUMPS ON THE RECIRCU-
                                                                                            PEDCo  ENVIRONMENTAL
                                                                                                   CINCINNATI. OHIO

-------
                                                WILL  COUNTY  UNIT  NO.  1  (CONTINUED)
 PERIOD    MODULE
MONTH/YEAR
    SYSTEM PERFORMANCE FACTORS  («)
AVAILABILITY   OPERMSILITY   RELIABILITY   UTILIZATION
JUN. 75
     64
     85
61
85
60
8"*
                                                                   75
JUL. 75
     79
                   79
                                77
                          7
-------
                                                WILL COUNTY UNIT NO. 1  (CONTINUED)
  PERIOD    MODULE
MONTH/TEAR
   SYSTEM PERFORMANCE FACTORS m
AVAILABILITY  OPEHA8ILITY  RELIABILITY  UTILIZATION
AUG. 75
    9«t
                                         100
                               92
                                            76
SEP. 75
    63
              63
                           63
OUT. 75
     32
100
26
                         COMMENTS


SULFUR COAL WAS BURNED DUKING THE FIRST (3) WEEKS


AND HIGH SULFUR ILLINOIS COAL WAS BURNED DURING


THE LAST WEEK OF THE MONTH.


MUQULE A REMAINED OUT OF SERVICE ALL MONTH. MODULE


B WAS SHUT DOWN SEVEN TIMES DURING THE MONTH, FOUR


OF WHICH WERE DUE TO »NO DEMAND.* HIGH SULFUR PILE


COAL WAS BURNED IN THE UNIT DURING THE MONTH.


RESULTING IN A SUBSTANTIAL INCREASE IN SLUDGE PHO.


DUCTION AND FORCING A 6-DAY, 10 HR/DAY, SLUDGE


DISPOSAL OPERATION.  SLUDGE STABILIZATION IS


CONTINUING.


MODULE A REMAINED OUT OF SERVICE ALL MONTH BECAUSE


OF DELAY ON THE NEW REHEATER ORDER.  MODULE B WAS


DOWN 8 TIMES BECAUSE OF MASSIVE ABSORBER SCALE,


DEMISTER AND I.D. BOOSTER FAN CLEANING, BALANCING


I.D. BOOSTER FAN, AND PLUGGING OF ABSORBER PUMP


SCREEN.  TOTAL OUTAGE TIME WAS 236 HOURS, to


MINUTES FOR CLEANOUT AND FAN BALANCING.  HIGH


SULFUR COAL WAS BURNED IN THE BOILER WHEN THE


SCRUBBER WAS IN THE GAS PATH.


ON OCTOBER 11, OVERHAUL BEGAN ON THE WILL COUNTY


UNIT NO. 1 BOILER, TURBINE,AND SCRUBBER. MODULE  B


EXPERIENCED TWO MINOR OUTAGES DURING THE 11-DAY


PERIOD PRIOR TO THE OVERHAUL.  MODULE A REMAINED
                                                                 69
                                                                                            PEDCo  ENVIRONMENTAL
                                                                                                   CINCINNATI. OHIO 45246

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                                                WILL COUNTY UNIT NO.  i (CONTINUED)
  PERIOD    MODULE
MONTH/YEAR
NOV. 75
            SYSTEM PERFORMANCE FACTORS (%)
        AVAILABILITY  OPEKABILITY  RELIABILITY  UTILIZATION
     TURBINE..  BOILER,  AND SCRUBBER OVERHAUL
DEC. 75
     TURBINE, BOILER AND SCRUBBER OVERHAUL
JAN. 76
FEB. 76
MAR. 76
     TURBINE, BOILER AND SCRUBBER OVERHAUL
     TURBINE, BOILER AND SCRUBBER OVERHAUL
A
B
SO
 9
                                         20
21
 8
19
 a
                         COMMENTS
OUT OF SERVICE PENDING DELIVERY OF THE NEW RE-
HEATEK
THE SCHEDULED OVERHAUL OF THE BOILER, TURBINE, AND
SCRUBBER MODULES CONTINUED.  MAJOR MAINTENANCE
AREAS INCLUDED MODULE REHEATERS, POND RETURN PUMP,
VENTURI SPRAY NOZZLES, VENTURI AND ABSORBER
MODULES, PUMP VALVES, AND SUMPS.
MODULE B REHEATER WAS RETURNED FROM MANUFACTURER
AFTER REPAIRS AND REVISIONS.  SCRUBBER REHEATERS
COULD BE INSTALLED AND OPERATING BY THE END OF
JANUARY.
THE UNIT REMAINED OUT OF SERVICE FOR COMPLETION OF
THE BOILER, TURBINE, AND SCRUBBER OVERHAUL THAT
BEGAN ON OCTOBER 11, 1975.  SYSTEM RESTART is NOW
SCHEDULED FOR MID-MARCH 1976.
UNIT NO. i RETURNED TO SERVICE IN MARCH FOLLOWING
THE EXTENDED MAJOR BOILER, TURBINE AND SCRUBBER
OVERHAUL.  THE A-SIDE WAS PUT INTO THE GAS PATH
ON MARCH 22 AND REMAINED AVAILABLE FOR SERVICE THE
REST OF THE MONTH.  THE B-SIDE REMAINED OUT OF
SERVICE UNTIL MARCH 29 BECAUSE OF DELAYS IN THE
INSTALLATION OF A REPAIRED REHEATER.  DURING MARCH
HIGH SULFUR ILLINOIS COAL WAS FIRED IN THE BOILER.
                                                                70
                                                                                           PEDCo  ENVIRONMENTAL
                                                                                                  CINCINNATI. OHIO

-------
                                                WILL COUNTY UNIT NO. 1  (CONTINUED)
  PERIOD    MODULE
MONTH/YEAR
    SYSTEM PERFORMANCE FACTORS (SI
AVAILABILITY  OPEHAblLITY  RELIABILITY  UTILIZATION
APR. 76
  A
  B
A S B*
23
51
                  20
                                         20
            20
19
                                            19
MAY  76
    87
65
             65
                                                      76
                         COMMENTS
DURING THE MONTH OF APRIL THE A-SIDE INCURRED PUMP
LINER FAILURES WHEN AN ISOLATION VALVE BROKE AND
FELL INTO THE VENTuRl RECYCLE PUMP. B-SIDE OUTAGES
DURING APRIL RESULTED FROM REHEATER TUBE BUNDLE
LLAKS* PLUGGED ABSORBER TANK SCREEN* AND VENTURI
PUMP LINER FAILURE.  HIGH SULFUR COAL u.s PERCENT
SULFUR) WAS BURNED IN THE BOILER THROUGHOUT THE
MONTH.  IN ADDITION. THE UTILITY INITIATED A
TESTING AND EVALUATION PROGRAM DURING THE MONTH.
THIS PROGRAM IS DESIGNED TO PROVIDE DATA AND
INFORMATION CONCERNING CHEMISTRY AND RELATED
OPERATING CHARACTERISTICS.
THE A-SIDE MAS DOWN THE ENTIRE MONTH AWAITING A
PARTS SHIPMENT (VENTURI PUMP LINERS).  MODULE B
ENCOUNTERED FOUR FORCED SCRUBBER OUTAGES.  THREE
OF THESE OUTAGES WERE MECHANICAL PROBLEMS, DUE
TO A VENTURI HOSE LEAK. PLUGGED ABSORBER TANK
SCREEN, AND A FOULED I.D. BOOSTER FAN.  HIGH
SULFUR ILLINOIS COAL WAS BURNED IN THE BOILER
DURING THE MONTH.  THE SLUDGE WAS STABILIZED WITH
LIME AND FLY ASH AND HAULED TO AN OFF-SITE
DISPOSAL AREA.
                                                                71
                                                                                           PEDCo  ENVIRONMENTAL
                                                                                                  CINCINNATI. OHIO  45246

-------
                                                WILL COUNTY UNIT NO. 1 (CONTINUED*
   PERIOD    MODULE
 MONTH/YEAR
              SYSTEM PERFORMANCE FACTORS m
          AVAILABILITY  OPEKABILITY  RELIABILITY  UTILIZATION
 JUN. 76
  A
  B
A S B*
 50
 63
85
37
                                                      81
JUL. 76
  A
  B
                          20
                          86
                0
               90
              0
             8<*
AUG. 76
  A
  B
A S B*
96
65
57
61
17
                                                      96
36
70
31
 0
72
                                                                   38
                                                                   11
                         COMMENTS
SIDE-A HAS RETURNED TO SERVICE JUNE 9 FOLLOWING
THE INSTALLATION OF A NEu VENTuRI PUMP LINER.
FOUR FORCED SCRUBBER OUTAGES WERE REPORTED-
TWO BECAUSE OF NO DEMAND, ONE FOR A BYPASS-
DAMPtR FAILURE AND ONE FOR I.D. BOOSTER FAN
FOULING.  THE B-SIDE ENCOUNTERED SEVERAL FORCED
SCRUBBER OUTAGES. TWO DUE TO NO DEMAND AND
SEVERAL SHORT TRIPS BECAUSE OF SCALING AND
PLUGGING IN THE VENTURI TANK SCREEN.  HIGH SULFUR
ILLINOIS COAL WAS BURNED IN THE BOILER DURING
THE MONTH.  SLUDGE FIXATION AND HAULAWAY TO A
DISPOSAL SITE CONTINUED.
THE A-SIDE REMAINED OUT OF SERVICE THE ENTIRE
MONTH BECAUSE OF REPAIRS TO A DAMAGED ABSORBER
PUMP AND POND THICKENER SLUDGE OVERLOADING.  THE
8-SIDE ENCOUNTERED FOUR FORCED SCRUBBER OUTAGES*
TWICE FOR NO DEMANDi ONCE TO BALANCE THE I.D.
BOOSTER FANS, AND ONcE To WASH THE I.D. BOOSTER
FANS.
THE A-SIDE REMAINED OUT OF SERVICE 50 PERCENT OF
Of- THE TIME DURING THE MONTH TO AVOID POND
THICKENER OVERLOADING.  FOUR SCRUBBER OUTAGES
WERE REPORTED*  ONE BECAUSE OF NO DEMAND AND THREE
BECAUSE OF MINOR PROBLEMS.  THE B-SlDE ENCOUNTERED
                                                                                          PEDCo  ENVIRONMENTAL
                                                                                                 CINCINNATI. OHIO .452^6

-------
                                                WILL COUNTY UNIT NO. 1 (CONTINUED)
  PERIOD    MODULE
MONTH/YEAR
    SYSTEM PERFORMANCE FACTORS (X)
AVAILABILITY  OPEHABILITY  RELIABILITY  UTILIZATION
SEP. 76
  A
  B
A X B*
42
79
29
76
 5
26
74
                                                                   60
                                                                                  COMMENTS
                                                         THREE NO-UEMAND OUTAGES, TWO BECAUSE OF LOSS OF
                                                         CHEMICAL CONTROL, ONCE FOR FOULING AND ONCE FOR
                                                         SPENT SLURRY VALVE REPAIRS.  EXPERIMENTATION WITH
                                                         THE SYSTEM'S PROCESS CHEMISTRY, BY LOWERING THE
                                                         PH SET POINT FROM 5.* TO 5.1. WAS CONDUCTED BY THE
                                                         UTILITY DURING THIS PERIOD.  THIS VARIATION IN
                                                         OPERATION WAS BELIEVED TO HAVE CAUSED THE MAS-
                                                         SIVE GYPSUM SCALING IN BOTH MODULES WHICH OCCURRED
                                                         DURING THE PERIOD.  THE PH SET POINT WAS RETURNED
                                                         BACK TO THE 5.t VALUE.  HIGH SULFUR ILLINOIS COAL
                                                         WAS BURNED IN THE BOILER DURING THE MONTH.  SLUDGE
                                                         STABILIZATION PRACTICES CONTINUED.
                                                         FIVE OUTAGE PERIODS WERE REPORTED DURING THE MONTH
                                                         FOR THE A-SIDE. THREE OF WHICH RESULTED FROM
                                                         FORCED SCRUBBER OUTAGES.  PROBLEMS WERE REPORTED
                                                         WITH LOW FLOW TRIPS IN THE VENTURI, NOZZLE FOULING
                                                         CLEANING AND INSPECTION OF THE RECIRCULATION TANK,
                                                         PUMPS AND VALVES, AND A PUMP MOTOR FAILURE.  THE
                                                         B-SIDE ENCOUNTERED FOUR FORCED SCRUBBER OUTAGES*
                                                         TWO BECAUSE OF SPENT SLURRY VALVE TROUBLE, ONE LOW
                                                         VENTURI FLOW TRIP AND ONCE BECAUSE OF LOSS OF
                                                         CHEMICAL CONTROL.  HIGH SULFUR ILLINOIS COAL
                                                         BURNING WAS CONTINUED IN THE BOILER DURING THE
                                                         MONTH.
                                                                73
                                                                                           PEDCo   ENVIRONMENTAL
                                                                                                  CINCINNATI. OHIO

-------
                                               WILL COUNTY UNIT NO.  1  (CONTINUED)
  PERIOD    MODULE
MONTH/YEAR
OCT. 76
NOV. 76
    SYSTEM PERFORMANCE  FACTORS  (X)
AVAILABILITY   OPERABILITY  RELIABILITY   UTILIZATION


A


A
A
B
* 8*
A
B
a B*
30
76
0
20
72

29
56
0
26
70
a
26
70
0
20
66

28
55
0
20
55
7
          •NOTE- ASB DESIGNATION AND  THE  CORRESPONDING  PERFORMANCE.
                VALUES REFER  TO THE  SIMULTANEOUS  OPERATION  OF
                BOTH  SCRUBBING TRAINS DURING  THE  REPORT  PERIOD
                IN QUESTION.
                                                                                  COMMENTS
                                                         PROBLEMS RELATED To THE A-SIOE SCRUBBER WERE DUE

                                                         PRIMARILY TO REPAIRS NECESSARY TO THE 1A1 RECYCLE

                                                         PUMP, AND DELAYS IN REPLACEMENT PARTS SHIPMENTS.

                                                         THE A-SIDE MODULE HAS IN SERVICE WHEN THE B-SIDE

                                                         WAS DOWN, HOWEVER SCRUBBING LIQUOR FLOW WAS

                                                         REDUCED BECAUSE ONLY ONE RECYCLE PUMP WAS IN USE.

                                                         AT THE END OF NOVEMBER. THE REMAINING A-SIDE PUMP

                                                         WAS TAKEN OUT OF SERVICE FOR OVERHAUL AND REPAIRS.

                                                         FOLLOWING THIS THE A-SIDE WILL RESUME OPERATIONS

                                                         ON ONE PUMP.

                                                         ON THE B-SIDE. 3 FORCED SCRUBBER OUTAGES OCCURRED

                                                         DURING OCTOBER.  ONE WAS BECAUSE OF REPAIRS OF A

                                                         REHEATER HEADER LEAK AND THE TIE-IN OF A VACUUM

                                                         FILTER AT THE THICKENER.  THE OTHER TWO RESULTED

                                                         FROM A VENTURI NOZZLE CLEAN-OUT AND A VENTURI LOW-

                                                         FLOW TRIP.  DURING NOVEMBER. "* SCRUBBER TRIPS

                                                         OCCURED BECAUSE OF A MILLING SYSTEM FAILURE, VEN-

                                                         TURI HEADER LEAK REPAIR AND VENTURI NOZZLE CLEAN-

                                                         ING, REPLACEMENT OF SPENT SLURRY VALVE, AND CHEM-

                                                         ICAL SYSTEM UPSET.  TWO OUTAGES WERE ALSO LOGGED

                                                         BECAUSE OF NO DEMAND.
                                                                                           PEDCo  ENVIRONMENTAL
                                                                                                  CINCINNATI. OHIO

-------
                                                 WILL  COUNTY  UNIT NO.  1  (CONTINUED)
  PERIOD    MODULE
MONTH/YEAR
            SYSTEM PERFORMANCE FACTORS  (X)
        AVAILABILITY  OPERABILITY  RELIABILITY  UTILIZATION
DEC. 76
A

B
                          53
              <*e

              52
            45

            51
 JAN. 77
 A

 B
98
99

 1
                            96

                             1
96

 1
                         COMMENTS

THE A-SIOE WAS PLACED IN SERVICE DURING THE LATTER

PART OF THE MONTH AND OPERATED CONTINUOUSLY WITH

THE EXCEPTION OF ONE MINOR OUTAGE FOR

SLURRY VALVE REPAIRS.  A SPENT SLURRY VALVE

FAILURE FORCED THE B-SIDE OUT OF SERVICE THE

REMAINDER OF THE MONTH.  SIMULTANEOUS MODULE OPER-

ATION TIME WAS 0 HOURS.  THE SCRUBBER MODULES ARE

SEEING SERVICE ON A  ROTATIONAL BASIS* I.E.* ONE

MODULE UP, ONE MODULE DOwN.  SLUDGE  STABILIZA-

TION  PRACTICES AND OPERATION ON  LOW  SULFUR COAL

CONTINUED  DURING THE MONTH.

ROTATIONAL MODULE OPERATIONS CONTINUED.  A-SiDE

FORCED OUTAGES*  SPENT SLURRY VALVE FAILURE AND

PLUGGED  DEMISTER UNOERSPRAYS.   THE DECEMBER SPENT

SLURRY VALVE FAILURE KEPT  THE  B-SIDE OUT OF SER-

VICE  UNTIL JAN.  27.  ACTUAL B-SIDE SERVICE TIME

WAS ONE  DAY.  SLUDGE STABILIZATION AND DISPOSAL

PRACTICES  CONTINUED. LOW  SULFUR WESTERN COAL WAS

BURNED IN  THE  BOILER.
                                                                 75
                                                                                           PEDCo  ENVIRONMENTAL.
                                                                                                  CINCINNATI. OHIO 45246

-------
                                               WILL COUNTY UNIT  NO.  1  (CONTINUED)
  PERIOD    MODULE
MONTH/YEAR
    SYSTEM PERFORMANCE FACTORS (X)
AVAILABILITY  OPEKABILITY  RELIABILITY  UTILIZATION
FEB.  77
                                                                  39
                           72
            A J B
                                            12
                         COMMENTS
DURING THE ENTIRE MONTH OF FEB. 1977i LOW-SULFUR
COAL WAS BURNED IN THE BOILER.  THERE WAS VERY
LITTLE DIGGING IN THE RECIRCULATION PONDS.  CHICAGO
FLYASH SPENT MOST OF THEIR TIME ON CLEANING AND
MAINTENANCE.
MODULE A WAS OFF THE FIRST PART OF THE MONTH FOR
CLEANING OF UNOERSPRAYS. OVERSPRATS AND ABSORBER
SPRAY NOZZELS.  PLUGGING WAS CAUSED BY A FAILED
CLASSIFIER LINER, WHICH ALLOWED OVERSIZED PARTICLES
TO ENTER THE SYSTEM.  THE CLASSIFIER LINER WAS RE-
PLACED.
MODULE B WAS FORCED OUT OF THE GAS PATH THREE TIMES
THIS MONTH.  THE REASONS WERE* HIGH VIBRATION OF
I.D. BOOSTER FAN, REPACKING OF IBl AND 1B2 ABSORBER
PUMPS. AND BEARING FAILURES IN A AND B SLURRY TRAN-
SFER PUMPS.

IN MARCH AN ERT soa ANALYZER WAS INSTALLED ON THE
DISCHARGE SIUE OF B MODULE I.D. BOOSTER FAN.  THIS
IS AN  *IN SITU* NON-DISPERSIVE ANALYZER THAT CON-
TINUALLY MEASURES AND READS OUT CONCENTRATIONS OF
S02, C02t CO AND NO.  HIGH-SULFUR COAL WAS BURNED
FOR SEVEN DAYS DURING MARCH TO PROVIDE HIGH SULFUR
                                                                                           PEDCo  ENVIRONMENTAL
                                                                                                  CINCINNATI. OHIO 45246

-------
                                                WILL COUNTY UNIT NO. 1  (CONTINUED)

                           SYSTEM PERFORMANCE FACTORS (X)
MONTH/YEAR                                                                                              COMMENTS

                                                                               SLUDGE FOR THE U.O.P. SLUDGE TEST  (A U.O.P. TEST

                                                                               CREW WAS EXPERIMENTING WITH POWERTON FLYASH AND

                                                                               HIGH-SULFUR SLUDGE).  CHICAGO FLYASH SPENT ABOUT

                                                                               75% OF THEIR TIME DIGGING  IN THE RECIRCULATION

                                                                               POND.  THE REST  WAS  SPENT  ON THE THICKENER AND

                                                                               VACUUM FILTER  OPERATIONS.  THE  SCRUBBER  WASTE

                                                                               MATERIAL WAS  TREATED WITH  LIME  AND FLYASH  AND HAUL-

                                                                               ED TO AN OFF-SITE DISPOSAL AREA.

 MAR. 77       A            97            66                        64          MODULE FORCED OUT OF THE GAS PATH  ONCE THIS  MONTH

                                                                                TO ALLOW FOR REPAIR TO A VENTURl  FLOW  DIFFERENTIAL

                                                                                LINE.

               B            ai            75                        73          MODULE FORCED OUT OF THE GAS PATH FOUR TIMES.   THE

                                                                                REASONS WERE* RUPTURED DIAPHRAM ON REHEATER  STEAM

                                                                                VALVE. ABSORBER SUCTION LEAK, SpENT SLURRY VALVE

                                                                                GASKET LEAK AND PLUGGED FEED SLURRY RECIRCULATION

                                                                                LINE.

              A ft B                        52                        51
                                                                 77

                                                                                       X   PEDCo  ENVIRONMENTAL
                                                                                                  CINCINNATI. OHIO 45246

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  PERIOD    MODULE
MONTH/YEAR
             SYSTEM PERFORMANCE FACTORS (*J
          AVAILABILITY  OPERABILITY  RELIABILITY
                                               WILL COUNTY  UNIT  NO.  1  (CONTINUED!

                                                               UILIZATION
APR. 77
  A
  B
A S B*
                          86
               68
               30
               23
HAY  77
  A
  B
A * B*
69
98
Z
51
 0
                          61
                          21
                          20
 2
«*7
 0
                                                                78
                        COMMENTS
2 OUTAGES WERE REPORTED FOR THE A-SIOE DURING
APRIL, ONE FOR A BOILER TUBE LEAK REPAIR. AND ONE
TO REPAIR A VENTURI THROAT LEAK.  B-SIOE OUTAGES
OCCURRED TWICE FOR ABSORBER SUCTION HEADER REPAIR,
AND ONCE TO WASH THE I.D. BOOSTER FAN. BOTH MOD-
ULES WERE FORCED OUT OF SERVICE APRIL 23 WHEN THE
SLURRY STORAGE TANK MIXER STRIPPED A PINION GEAR.
PREPARATIONS ARE BEING MADE FOR MGD ADDITION AND
FORCED OXIDATION TEST.  THE ERT S02 ANALYZER PER-
FORMANCE HAS BEEN INCONSISTENT PRIMARILY DUE TO A
FAULTY CIRCUIT.  HIGH-SULFUR COAL WAS BURNED FOR
SEVEN DAYS AND SLUDGE STABILIZATION PRACTICES IN-
VOLVING LIME AND FLYASH TREATMENT WERE CONTINUED
DURING THE MONTH.
A-SIDE OUTAGE OCCUREO ONCE DURING MAY DUE TO INLET
VALVE FAILURE ON THE 1A2 ABSORBER PUMP.  THE
B-SIDE MODULE WAS TAKEN OFF FOR INSPECTION AND
CLEANING OF THE REHEA*ER TUBES.  TRANSFORMER FAIL-
URE ON THE POND RETURN PUMPS KEPT BOTH SIDES OUT
OF SERVICE FOR THE FIRST 15 DAYS OF THE  MONTH.
THE ERT S02 ANALYZER HAS BEEN  REMOVED FROM SERVICE
DUE TO POOR PERFORMANCE.   HIGH-SULFUR COAL WAS
BURNED FOR ELEVEN DAYS FOR THE MGO  TEST, WHICH
WENT  WELL.  RESULTS SHO* ABOUT 10 PERCENT GREATER
S02 REMOVAL EFFICIENCY WITH THE MG  ION ADDITION,
                                                                                           PEDCo  ENVIRONMENTAL
                                                                                                  CINCINNATI. OHIO  45246

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                BUT NO IMPROVEMENT FOR THICKENER  OR  SLUDGE PRO-

                DUCTION  PHOBLtMS.   THE LIMESTONE  CONSUMPTION  RATE

                WAS ABOUT  THE  SAME.  SLUDGE  STABILIZATION  AND  DIS-

                POSAL  PRACTICES  CONTINUED.   THERE WAS  NO  SIMUL-

                TANEOUS  OPLRATON OF  A  AND B SCRUBBER MODULES.
79
                /^~^\
                         PEDCo  ENVIRONMENTAL
                                CINCINNATI. OHIO  45246

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                  TABLE:  5
PERFORMANCE DESCRIPTION  FOR  OPERATIONAL  FGO  SYSTEMS   06/77
 IDENTIFICATION NO.

 UTILITY NAME

 UNIT NAME

 UNIT LOCATION

 UNIT RATING
  31


 QUQUESNE LIGHT


 ELRAMA  POWLR STATION


 ELRAMA  PENNSYLVANIA


  510 MW
 FUEL CHARACTERISTICS   COAL   1.0  -  2.8  PERCENT  SULFUR
 FGO VENDOR

 PROCESS

 NEW OR RETROFIT

 START UP  DATE

 FGD STATUS

 EFFICIENCYt
  PARTICULATES
 CHEMICO


 LIME SCRUBBING


 RETROFIT


 10/75


 OPERATIONAL



 99 PERCENT
  S02
 63 PERCENT DESIGN - 2% S COAL
 WATER MAKE UP
 OPEN LOOP
 SLUDGE DISPOSAL
  STABILIZED SLUDGE DISPOSED IN  UNLINED POND
 UNIT COST
$93/KW CAPITAL * 6 MILLS/KWH OPERATING COSTS (BOTH STATIONS)
 OPERATIONAL
  EXPERIENCE
 REFER TO THE BACKGROUND INFORMATION SECTION IN TABLE 5 OF THIS REPORT.
 OPERATIONS ARE CONTINUING WITH TWO BOILERS COUPLED INTO THE FIVE-MODULE
 SCRUBBING SYSTEM. RUBBER-LINED RECYCLE PUMPS HAVE BEEN REMOVED FROM TEST.
 ING AS THEY WERE UNDERGOING SEVERE ABRASION AND GOUGING. ANOTHER SET OF
 RUBBER-LINED PUMPS MAY BE TESTEOt SCRUBBING WASTES ARE CHEMICALLY FIXATED
 BY THE iucs METHOD ANU LANOFILLED. DUQUESNL LIGHT is CONTINUING EFFORTS
 TO OBTAIN ALTERNATE LANDFILL AREAS AS THE CURRENT ONES ARE BEING FILLED
 FAIRLY RAPIDLY.
                                                             ao
                                                                                       PEDCo  ENVIRONMENTAL

                                                                                              CINCIIMNATI. OHIO  45246

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                                                      BACKGROUND INFORMATION

                                                                ON

                                                       ELRAMA POWER STATION

     DUQUESNE LIGHT COMPANY. AN IrtVESTOR-OWNED ELECTRIC UTILITY, SERVES ABOUT ONE-HALF MILLION CUSTOMERS IN SOUTHWESTERN

PENNSYLVANIA AND HAS A NET GENERATING CAPABILITY OF APPROXIMATELY 2500 MW.  THIS CAPABILITY IS GENERATED BY COMBUSTION TURBINES IN

SIMPLE AND COMBINED-CYCLE MODES, BY NUCLEAR PLANTS, AND BY COAL-FIRED POWER STATIONS,   THE COMPANY IS SOLE OWNER AND OPERATOR OF

THREE COAL-FIRED STATIONS, TWO OF WHICH HAVE BEEN RETROFITTED WITH WET SCRUBBERS USING LIME AS THE ABSORBING REAGENT.

     THE SCRUBBER FACILITY AT THE «»9«»-MW ELRAMA STATION IS ALMOST IDENTICAL TO THE SYSTEM AT THE PHILLIPS STATION.   GIBBS X HILL

IS THE A-E FIRM AND CHEHICO SCRUBBERS HAVE BEEN INSTALLED WITHIN THE SAME DESIGNATED BATTERY LIMITS AS AT PHILLIPS.  MECHANICAL

AND ELECTRICAL DUST-REMOVAL EQUIPMENT REMOVES MOST PARTICULATES FROM THE BOILER EMISSIONS, AND THE GAS To AND FROM  THE SCRUBBERS

IS HEADEREO IN THE SAME WAY.  UNLIKE THE PHILLIPS SYSTEM, HOWEVER, THERE ARE FOUR BOILERS, EACH WITH ITS OWN TURBINE GENERATOR.

FIVE SINGLE-STAGE SCRUBBERS WERE INSTALLED, WITH THE INTENTION THAT KNOWLEDGE GAINED FROM THE TEST PROGRftM AT PHILLIPS WOULD BE

APPLIED TO ELRAMA To ENABLE COMPLIANCE WITH EMISSION REGULATIONS.

     THE FIRST ELRANA SCRUBBER WAS PLACED IN SERVICE ON OCTOBER 26, 1975.  IT HAD BEEN SCHEDULED FOR AN EARLIER STARTUP DATE, BUT

BECAUSE OF THE SEVERITY AND NUMBER OF PROBLEMS ENCOUNTERED AT PHILLIPS, STARTUP WAS DELAYED UNTIL MANY OF THE PROBLEMS AT PHILLIPS

WERE RESOLVED AND THE MODIFICATIONS COULD BE INCORPORATED AT BOTH STATIONS.

     BOILER NO. 2 WAS INITIALLY CONNECTED TO THE FGD SYSTEM ON OCTOBER 26, 1975.  THIS BOILER HAS AN EQUIVALENT CAPACITY  OF

APPROXIMATELY 100 MW, AND THE EMISSIONS ARE.HANDLED BY ONE SCRUBBER.  TO ENSURE RELIABILITY IN THE CASE OF A SCRUBBER MALFUNCTION,

TWO SCRUBBERS ARE OPERATED AT PARTIAL LOAD TO PROTECT THE BOILER AND TURBINE GENERATOR AGAINST A TRIP-OFF.

     THE BOILER OPERATED CONTINUOUSLY ON THE SCRUBBER SYSTEM THROUGH JANUARY 1976.  TWO MINOR OUTAGES OCCURRED DURING THIS PERIOD,

ONE CAUSED BY INOPERATIVE THROAT DAMPERS AND THE OTHER INVOLVING FAILURE OF A LIME FEEDER BELT. ON FEB. «»,1976, A SECOND BOILER

WAS COUPLED INTO THE SCRUBBER COMPLEX. PRESENTLY, 2 UNITS ARE THE MAXIMUM THAT CAN BE TIED INTO THE SCRUBBER PLANT.  TO DATE,

THE UTILITY HAS ENCOUNTERED THE USUAL MINOR STARTUP PROBLEMS AND SOME MAJOR PROBLEMS AS WELL.  THE MAJOR PROBLEMS HAVE BEEN

FROZEN PIPES AND THICKENERS, THE LATTER INVOLVING HARDWARE AND DESIGN ASSOCIATED WITH RECIRCULATION OF THE SLUDGE WITHIN THE

THICKENERS TO ATTAIN 30 TO 40 PERCENT SOLIDS CONCENTRATION.

     THE SLUDGE BEING GENERATED AT THIS STATION is TREATED BY THE lues METHOD, WHICH EMPLOYS A VACUUM FILTER THAT INCREASES THE

SOLIDS IN THE UNDERFLOW TO 50 TO 60 PERCENT, SO THAT LESSER AMOUNTS OF OR* FLY ASH ARE REQUIRED FOR MIXING WITH THE SLUDGE.
                                                                61

                                                                                           PEDCo  ENVIRONMENTAL-
                                                                                                 CINCINNATI. OHIO 45246

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PERIOD
OCT. 75
  TO
JAN. 76
FEB. 76
MAR. 76
APR. 76
HAY  76
JUN. 76
JUL. 76
AUG. 76
SEP. 76
    OPERATING HOURS
BOILER            SCRUBBER VESSELS
             1169  1508   976
638
ELRAMA POWER STATION
                                   COMMENTS
     ONE BOILER WAS CONNECTED TO THE SCRUBBER SYSTEM ON OCTOBER 26t 1975.
     A SECOND BOILER WAS CONNECTED ON FEBRUARY <*, 1976.  FOUR OF THE
     SCRUBBER VESSELS HAVE BEEN IN SERVICE IN VARIOUS COMBINATIONS.  THE
     SERVICE HOURS TO JANUARY 31t 197i» ARL POSTED IN THE ACCOMPANYING
     TABLE.  THE FIFTH VESSEL HAS NOT BEEN IN SERVICE BECAUSE IT IS BEING
     REVISED FOR TRIAL INSTALLATION OF RUBBER-LINED RECYCLE PUMPS.
     THE SYSTEM OPERATED DURING THE REPORT PERIOD WITH 2 BOILERS COUPLED
     INTO THE SCRUBBING SYSTEM.  REVISIONS TO THE FIFTH SCRUBBING VESSEL
     HAVE BEEN COMPLETED AND OPERATIONS ARE PROCEEDING WITH TWO RUBBER-
     LINED RECYCLE PUMPS.
     THE SYSTEM IS STILL OPERATING WITH TWO BOILERS COUPLED INTO THE
     SCRUBBING SYSTEM.  THE FIFTH SCRUBBING VESSEL WAS TAKEN OUT OF SERVICE
     FOR REPAIRS AND MODIFICATIONS REOUIREP FOR THE RUBBER-LINED RECYCLE
     PUMPS.  THE UTILITY IS CURRENTLY CONDUCTING A PERFORMANCE TEST ON
     THE SCRUBBING SYSTEM IN THE TWO BOILER OPERATION MODE.  THE IUcS
     SLUDGE FIXATION SYSTEM is STILL OPERATING AT THIS STATION.
     THE FIFTH SCRUBBING VESSEL EMPLOYING TWO RUBBER-LINED RECYCLE PUMPS
     WAS OPERATIONAL FOR A SHORT PERIOD OF TIME DURING THE REPORTING
     MONTHS.  TWO BOILERS REMAIN COUPLED  INTO THE SCRUBBING SYSTEM.  THE
     CONSTRUCTION OF ADDITIONAL E8UIPMENT AT THIS FACILITY IS CONTINUING.
     ADDITIONAL LIME STORAGE SILOS AND A  THICKENER WILL BE REQUIRED
     FOR FULL SCALE OPERATION.  THE UTILITY HAS SIGNED A LETTER OF INTENT
     WITH IUCS FOR A LONG-TERM SLUDGE FIXATION SYSTEM.  HIGH CALCIUM LIME
     IS STILL BEING EMPLOYED IN THE SCRUBBING SYSTEM.
     OPERATIONS AT THIS STATION DURING THE REPORT PERIOD PROCEEDED WITH
                                                                                          PEDCo  ENVIRONMENTAL
                                                                                                 CINCINNATI. OHIO

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                                               CLRAHA POWEfl STATION (CONTINUED)
PERIOD
OCT. 76
         OPERATING HOURS
               BOILER
SCRUBBER VESSELS
NOV. 76
DEC. 76
                              COMMENTS
TUO BOILERS COUPLED INTO THE 5-MODULE SCRUBBING SYSTEM.  THE 5TH
SCRUBBING VESSEL WAS OPERATIONAL DURING THE REPORT PERIOD WITH THE
RUBBER-LINED RECYCLE PUMPS IN SERVICE.  TESTS WERE CONDUCTED DURING
THE PERIOD TO DETERMINE PARTICULATE AND S02 REMOVAL EFFICIENCIES.  S02
REMOVAL EFFICIENCY WAS 50 PERCENT.  PARTICULATE EMISSIONS WERE BEING
REDUCED WELL BELOW THE 0.1 LB/MM BTU STANDARD (ACTUAL RESULTS*  0.0<4
LB/MM BTU).  THESE RESULTS WERE BASED ON 2 BOILERS COUPLED INTO THE 5
SCRUBBING MODULES WHILE BURNING MEDIUM-SULFUR (1.0 TO 2.8 PERCENT)
COAL.  THE MECHANICAL COLLECTORS AND ESP'S WERE IN SERVICE DURING
THE TESTS.  OPERATIONS ARE STILL PROCEEDING ON AN OPEN-WATER-LOOP
BASIS.  PART OF THE THICKENER OVERFLOW IS STILL BEING DIVERTED To THE
ASH POND AND NOT RECYCLED BACK TO THE PROCESS.  BECAUSE BOTH THE
BEAVER VALLEY AND BRUCE MANSFIELD STATIONS ARE FULLY OPERATIONAL,
THIS STATION HAS BEEN RELEGATED TO PEAK LOAD OPERATIONS.  GENERAL LOAD
OPERATIONS ARC FULL LOAD CAPACITY IN THE DAYTIME AND 50 TO 60 PERCENT
LOAD REDUCTION AT NIGHT.
THE SCRUBBER REMAINED IN SERVICE THROUGHOUT THE REPORT PERIOD WITH
TWO BOILERS COUPLED INTO THE SCRUBBING SySTEM.  RECYCLE PUMP EVALUA-
TION IS BEING CONDUCTED BY THE UTILITY AT BOTH THE PHILLIPS AND
ELRAMA STATIONS.  OBSERVATIONS OF THE RUBBER-LINED RECYCLE PUMPS
INDICATE SOME SEVERE ABRASION AND GOUGING HAVE OCCURRED AFTER 1000
HOURS OF SERVICE TIME.
                                                                                           PEDCo  ENVIRONMENTAL
                                                                                                 CINCINNATI. OHIO 452.46

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                                                ELRAMA POWER STATION  (CONTINUED)
                   OPERATING HOURS
PERIOD         BOILER             SCRUBBER VESSELS                                         COMMENTS
JAN. 77                                                     THE SCRUBBER PLANT CONTINUED OPERATIONS DURING THE REPORT PERIOD WITH
FEB. 77                                                     TWO BOILERS COUPLED INTO THE SYSTEM. TESTING ON THIOSORBlC LIME WAS
«AR. 77                                                     CONDUCTED  DURING THE PERIOD. INSTALLATION OF THE ADDITIONAL THICKENERt
                                                            LIME FEEDERS AND SILOS  IS STILL IN PROGRESS. FULL COMPLIANCE OPERATION
                                                            FOR THIS STATION IS SCHEDULED FOR EARLY 1976. THE FULL COMPLIANCE
                                                            STRATEGY WILL CONSIST OF THE FOLLOWING* 83* S02 REMOVAL FOR 2* SULFUR
                                                            COAL UTILIZING THIOSORBlC LIME <6-12*MG), FIXATING THE SCRUBBER
                                                            SLUDGE WITH THE IUCS POZ-0-TEC STABILIZATION METHOD AND HAULING
                                                            THIS MATERIAL TO AN OFF-SITE DISPOSAL/LANDFILL AREA. CURRENT S02 AND
                                                            PARTICULATE REMOVAL EFFICIENCIES ARE 50 AND 99+«, RESPECTIVELY. THE
                                                            INTERIM IUCS UNIT NOW IN SERVICE CONSISTS OF THE OLD MOHAVE PROTOTYPE
                                                            PLUS A VACUUM FILTER. THE STABILIZED MATERIAL HAS BEEN UTILIZED IN
                                                            A PARKING  LOT CONSTRUCTION PROJECT. IUCS HAS BEEN AWARDED A 10-YEAR
                                                            CONTRACT FOR THE CONTINUED USE OF THIS SYSTEM FOR FUTURE PLANT
                                                            OPERATIONS.
APR. 77                                                     CONSTRUCTION OF TWO 120-FOOT DIAMETER THICKENERS IS CONTINUING. DUE
MAY  77                                                     TO THE GOUGING OF THE RUBBER-LINED RECYCLE PUMPS DURING THEIR TESTING,
                                                            THEY HAVE  BEEN REMOVED. THE UTILITY IS CONSIDERING TRYING ANOTHER SET
                                                            OF RUBBER-LINED PUMPS,  OUQUESNE LIGHT ALSO IS CONTINUING EFFORTS TO
                                                            OBTAIN ALTERNATE LANDFILL AREAS FOR SLUDGE DISPOSAL.
                                                                                         PEDCo  ENVIRONMENTAL
                                                                                                CINCINNATI. OHIO

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                  TABLE 5
PERFORMANCE DESCRIPTION FOR OPERATIONAL F6D SYSTEMS  06/77
 IDENTIFICATION NO.

 UTILITY NAME

 UNIT NAME

 UNIT LOCATION

 UNIT RATING

 FUEL CHARACTERISTICS

 FGO VENDOR

 PROCESS

 NEW OR RETROFIT

 START UP DATE

 FGD STATUS

 EFFICIENCY.
  PARTICULATES
  32

 DUOUESNE LIGHT

 PHILLIPS POWER STATION

 SOUTH HEIGHT PENNSYLVANIA

  410 nw

 COAL   1.0- 2.8 PERCENT  SULFUR

 CHEM1CO

 LI«E SCRUBBING

 RETROFIT

  7/73

 OPERATIONAL


 99 PERCENT
  S02
 83 PERCENT DESIGN - 2* S COAL
 WATER HAKE UP
 OPEN LOOP
 SLUDGE DISPOSAL
 UNIT COST
  STABILIZED SLUDGE DISPOSED IN  UW.INED POND
S103/KW CAPITAL * 6 MILLS/KWH OPERATING COSTStBOTH STATIONS)
 OPERATIONAL
  EXPERIENCE
 REFER TO THE BACKGROUND INFORMATION SECTION IN TABLE 5 OF THIS HEPORT.
 THIS SCRUBBING SYSTEM HAS BEEN IN SERVICE SINCE JULY 1973. FOUR BOILERS
 CURRENTLY ARE COUPLED INTO THE SCRUBBING SYSTEM. THE OTHER TWO BOILERS
 ARE DOWN FOR MAINTENANCE. THE SCRUBBER SYSTEM MAS SHUT UQWN FOR ABOUT H
 DAYS IN MAY DUt TO LEAKING IN THE WET GAS HEADER THAT CONNECTS THE STACK.
 OVERALL SCRUBBER AVAILABILITY HAS BEEN ABOUT 75 PERCENT DURING THE RE-
 PORTING PERIOD. DEWATERED SLUDGE FROM THE IUCS INTERIM PROCESSING PLANT
 IS BEING HAULED TO AN OFF.SITE LANDFILL. THE SLUDGE CONTAINS NO FIXATIVE.
                                                                                         PEDCo  ENVIRONMENTAL
                                                                                                CINCINNATI. OHIO 45246

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                                                      BACKGROUND INFORMATION
                                                                ON
                                                      PHILLIPS POWER STATION
     THE PHILLIPS POWER STATION IS LOCATED ON THE OHIO RIVE" ABOUT 20 MILES NORTHWEST OF PITTSBURGH.  THE POWER STATION CONSISTS
OF SIX COAL-FIRED BOILERS HAVING A NET GENERATING CAPABILITY OF 387 MW.  THE RESULTANT FLUE GASES ARE DISCHARGED TO A COMMON
HEADER, TO WHICH THE FGD MODULES ARE CONNECTED THROUGH ISOLATION VALVES.  THE BOILERS ARE CURRENTLY BURNING COAL WITH A HEATING
VALUE OF 11,350 BTU PER POUND AND SULFUR AND ASH CONTENTS OF 2.2 AND 18.2 PERCENT, RESPECTIVELY.
     THE FGO SYSTEM, WHICH SUPPLEMENTS THE EXISTING MECHANICAL AND ELECTROSTATIC DUST COLLECTORS, CONSISTS OF FOUR TRAINS OF WET
VENTURI-TYPE SCRUBBERS. INSTALLED AT A COST OF APPROXIMATELY S103/KW.  GIBBS & HILL, INC.* WAS ENGAGED AS THE A-E FIRM FOR THE
ENTIRE PROJECT. BATTERY LIMITS OF THE CHEMICO CORPORATION ARE CONFINED TO THE SCRUBBERS AND ASSOCIATED PUMPS AND CONTROLS BETWEEN
THE INLET HOT GAS DUCT MANIFOLD AND THE EXIT WET GAS HEADER (INCLUDING THE REHEATER, EXCLUDING THE NEW ID FANS).
     THE FOUR TRAINS ARE LOCATED DOWNSTREAM OF EXISTING MECHANICAL COLLECTORS AND ESP'S INSTALLED IN SERIES ON EACH OF THE SIX
PULVERIZED-COAL-FIRED BOILERS. THREE OF THE TRAINS A«E SINGLE-STAGE VENTUHI SCRUBBERS ORIGINALLY INTENDED FOR PANICULATE REMOVAL.
THE FOURTH TKAIN IS A DUAL-STAGE VENTURI SCRUBBER-ABSORBER AND IS THE PROTOTYPE FOR DETERMINING THE FEASIBILITY OF TWO-STAGE
SCRUBBING FOR COMPLIANCE WITH SULFUR DIOXIDE EMISSION LIMITS. A DIAGRAM OF THE SCRUBBER-ABSORBER TRAIN INSTALLED AT THE PHILLIPS

STATION IS PRESENTED IN APPENDIX B.
     EACH TRAIN IS EQUIPPED WITH A NEW UET-TYPE ID FAN.  A NEW COMMON DUCT DIRECTS GAS STREAMS FROM Al* BOILERS TO THE SCRUBBER
SYSTEM. WHERE THEY CAN BE SENT TO ANY OR ALL OF THE TRAINS.  THE SCRUBBED GAS is EXHAUSTED THROUGH A COMMON DUCT AND AN OIL-FIRED
REHEATER TO A NEW GROUND-SUPPORTED STACK, WHICH CONTAINS AN ACID-RESISTANT BRICK LINER.
     SLAKED QUICKLIME IS ADDED TO THE LOWER CONE OF EACH OF THE SCRUBBER VESSELS TO NEUTRALIZE THE REClRcULATlNG LIQUOR, WHICH, IN
SINGLE-STAGE SCRUBBING WITH HIGH-CALCIUM LIME, REACTS WITH APPROXIMATELY 50 PERCENT OF THE SULFUR DIOXIDE IN THE FLUE GAS.  A
LIQUOR BLEED FLOW OF APPROXIMATELY H PERCENT IS SENT TO ONE OR BOTH OF THE THICKENERS FOR REMOVAL OF SOLIDS.  THE OVERFLOW IS
RETURNED TO THE SYSTEM AND THE UNDERFLOW is DISCHARGED TO THE iucs SLUDGE FIXATION SYSTEM. THIS INTERIM SLUDGE FIXATION SYSTEM
COMMENCED OPERATIONS IN DECEMBER 1976. THE FACILITY INCLUDES DEWATERING EQUIPMENT AND FLY ASH ADDITION EQUIPMENT  (COLLECTED
FROM THE ESP).  THE FIXATED MATERIAL IS THEN HAULED AWAY TO AN OFF-SITE LANDFILL AREA.
     FLUE GASES FROM THE BOILERS ARE ACCELERATED TO A HIGH VELOCITY IN THE SCRUBBER.  AT THE THROAT. THE GASES COLLIDE WITH THE
SCRUBBING LIQUID, ATOMIZING IT INTO SMALL DROPLETS.  THE FLY ASH AND THE SULFUR DIOXIDE IN THE GAS ARE PICKED UP BY THE SLURRY
DROPLETS AND EXIT AT THE BASE OF THE TOWER.  THE GAS THEN REVERSES DIRECTION AND FLOWS UP THROUGH THE MIST ELIMINATOR. WHERE FINE
                                                                86

                                                                                          PEDCo  ENVIRONMENTAL
                                                                                                 CINCINNATI. OHIO 45246

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PHILLIPS POWER STATION (CONTINUED)

DROPLETS ARC REMOVLD BEFORE THE GAS LEAVES THE SCRUBBER.

     STARTUP OF A PORTION OF THE PHILLIPS SCRUBBER SYSTEM BEGAN JULY 1973.  SEVERAL PROBLEMS THEN DEVELOPED IN THE FORM OF EROSION

OF FANS AND THE LIME FEED SYSTEM-. CAUSING OUTAGES OF THE SCRUBBER SYSTEM.  AFTER AN EXTENDED OUTAGE. THE SCRUBBER SYSTEM WAS

RETURNED TO SERVICE IN MARCH i97«».  THE SYSTEM HAS BEEN OPERATING CONTINUOUSLY SINCE THAT TIME WITH VARIOUS NUMBERS OF BOILERS

CONNECTED TO THE SCRUBBER SYSTEM AND SCRUBBER TRAINS IN SERVICE.

     DETERMINATION OF THE AVAILABILITY OF THE PHILLIPS SYSTEM HAS BEEN DIFFICULT.  UNTIL «LL BOILERS WERE CONNECTED TO THE SCRUB-

BERS. THERE WAS AT LEAST ONE SPARE TRAIN AND AS MUCH AS 100 PERCENT SPARE SCRUBBER CAPACITY.  THEREFORE. HAVING A TRAIN OUT OF

SERVICE FOR MAINTENANCE DID NOT REDUCE THE CAPABILITY OF THE SCRUBBER SYSTEM.  UNTIL ALL SIX BOILERS WERE CONNECTED. MEANINGFUL

AVAILABILITY FACTORS COULD NOT BE COMPUTED.  ON MARCH 17, 1975, THE SIXTH BOILER WAS CONNECTED, AND ALL FOUR SCRUBBER TRAINS WERE

REQUIRED TO BE IN SERVICE.  OPERATION IN THAT MODE CONTINUED UNTIL AUGUST 
-------
                                                           PHILLIPS POWER STATION
                          OPERATING HOURS
                    BOILER
MONTH      1     2     3     •»      5
JUL. 75   63    6<»<»  7()3   3<»9    605
AUG.  75  35«»     701
SEP. 75  «»63
OCT. 75  5H7
                287  669   503
                575  620   601*
NOV. 75   16
DEC. 75  172
                720   668
                660   709
70
 0
JAN. 76  222
                722  639
                                                    SCRUBBER-ABSORBER
                                                  101     201    301     401
                                                 HOO     160    531    723
                           "»57    517    
-------
                                                     PHILLIPS POWER STATION (CONTINUED)
MONTH
                    BOILtR
                 2     3
                          OPERATING HOURS
                                    SCRUBBER-ABSORBER
                                  101     201     301     fOl
FEB. 76  «*<»3
MAR. 76
APR.76
568  672
633
       571
 657   662
695    353
                                               166
                                               659
H06
H61
HAY  76
JUN. 76
                          COMMENTS
INCLUDED 1612 SERVICE HOURS ON ONE TRAIN AND 1309
HOURS ON ANOTHER TRAIN.  RESULTS INDICATE THAT
THE REQUIRED DEGREE OF So2 REMOVAL (83 PERCENT)
CAN BE OBTAINED WITH AN MGO CONTENT OF 8-10
PERCENT IN THE LIME? WITH SINGLE-STAGE SCRUBBING.

PLANT OPERATION IS PROCEEDING WITH A TOTAL OF t
BOILERS COUPLED INTO THE SCRUBBING SYSTEM
(EQUALING 336 MW, WHICH IS 67 PERCENT OF THE TOTAL
PLANT CAPACITY).  THE FGD SYSTEM OPERATED ON HIGH
CALCIUM LIME DURING THE REPORT PERIOD.  THE
GENERAL OPERATION MODE AT THIS FACILITY HAS ONE OF
THE FOUR SCRUBBING TRAINS OUT CONTINUALLY FOR
REPAIRS. CLEANING. AND PREVENTATIVE MAINTENANCE.
THE UTILITY IS STILL EXPERIENCING PROBLEMS WITH
SOLIDS DEPOSITION IN THE VENTURI THROAT OF THE
SCRUBBING MODULE. CAUSING MOVEMENT INHIBITION AND
GREATER PRESSURE DROPS.THE FGD SYSTEM AVAILABILITY
FOR THE FIRST QUARTER OF 1976 WAS 72 PERCENT.  THE
SLUDGE STABILIZATION PRACTICES ARE STILL
CONTINUNING AT THIS FACILITY.
REDUCED LOAD OPERATIONS WERE REPORTED BY THE
UTILITY FOR THE MAY-JUNE PERIOD BECAUSE OF A
                                                                89
                                                                                          PEDCo   ENVIRONMENTAL
                                                                                                 CINCINNATI. OHIO

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                                                    PHILLIPS POWER STATION  (CONTINUED)
MONTH
                    BOILER
                 a     3
                          OPERATING  HOURS
  SCRUBBER*ABSORBER
101    201    301    401
JUL.  76
AUG.  76
                                                                90
                          COMMENTS
SCHEDULED TURBINE OVERHAUL TO UNIT NO. 6.  THE
SCRUBBING SYSTEM WAS SHUT DOWN ON JUNE 27 FOR A
SCHEDULED FOUK *EE« REPAIR PERIOD.  THE MAJORITY
OF THE WORK WILL BE CONCENTRATED ON THE STACK,
ASSOCIATED DUCTWORK. AND BOILER DAMPERS.  ALSO,
THE UTILITY IS PROCEEDING WITH THE INSTALLATION OF
3 ADDITIONAL LIME STORAGE SILOS AND * THIRD
THICKENER.
THE H-WEEK SYSTEM OVERHAUL WAS COMPLETED JULY 25.
DURING THIS PERIOD, THE FOLLOWING REPAIRS AND
MODIFICATIONS WERE MADE*
     REPAIR OF THE TURNING VANES TO THE SCRUBBER
     DEMISTER.
     REPAIR OF THE EXPANSION JOINT SEAL WHERE THE
     DUCTWORK TIES INTO THE MAIN STACK.
     REPAIR OF STEEL BANDS AROUND INNER STACK
     STRUCTURE.
     OVERHAUL OF I.D. FANS.
     REPAIR OF BOILER EXIT DAMPERS.
     REPAIR LEAKAGE OF THE ACID-BRICK LINING IN
     THE MAIN STACK.
THE THREE ADDITIONAL LIME STORAGE SILOS AND THE
FOUNDATION FOR THE ADDITIONAL 75-FOOT DIAMETER
THICKENER HAVE BEEN INSTALLED.  THE UTILITY
HAS SIGNED A LETTER-OF-INTENT WITH IUCS FOR A
                                                                                           PEDCo  ENVIRONMENTAL
                                                                                                  CINCINNATI. OHIO

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                                                           PHILLIPS  POW£K
                                                                           .-,-. riON (CONTINUED!
MONTH


SEP. 76
OCT. 76
                    BOILER
                 2     3
                          OPERATING HOURS
  SCRUBBER-ABSORBER
101
201
           TOTAL SCRUBBER HOURS* 23*27*
           TOTAL BOILER HOURS* 83.6S2
           TOTAL SCRUBBER OUTAGE TIME* 5.500
           TOTAL SCRUBBER AVAILABILITY HOURS. 23.274
           AVERAGE MM LOAD/ SCRUBBER OPERATION HOUR* 2"»3
           TOTAL OPERABILITY INDEX* 26 PERCENT
                                                                91
"»01                                COMMENTS
    LONG-TERM SLUDGE TREATMENT SYSTEM.
    BOILCH NOS. 2-6 UEKE COUPLED INTO THE SCRUBBING
    SYSTEM.  BOILER NO. 1 IS DOWN FOR OVERHAUL AND
    REPAIRS.  THE iocs INTERIM SLUDGE PROCESSING
    PLANT IS UNDER CONSTRUCTION AND WILL BE IN SERVICE
    BY DECEMBER 1976.  THE TEMPORARY FACILITIES WILL
    PROCESS THE THICKENER UNDERFLOW AND PONDED
    SLUDGE UNTIL THE POND IS DEPLETED OF SLUDGE AND
    THE PERMANENT FACILITY HAS BEEN INSTALLED.
    SCRUBBING OPERATIONS ARE STILL PROCEEDING IN AN
    OPEN-WATER-LOOP MODE WITH PART OF THE THICKENER
    OVERFLOW BEING DIVERTED To THE ASH POND.
    BECAUSE BOTH THE BEAVER VALLEY AND BRUCE MANSFIELD
    STATIONS ARE FULLY OPERATIONAL. THIS STATION HAS
    BEEN RELEGATED TO PEAK LOAD OPERATIONS.  GENERAL
    LOAD OPERATIONS ARE FULL LOAD CAPACITY IN THE
    DAYTIME AND 50 TO 67 PERCENT LOAD REDUCTION AT
    NIGHT.
    THE FIGURES IN THE LEFT-HAND COLUMNS HAVE BEEN
    COMPILED BY THE UTILITY FOR SYSTEM OPERATIONS FOR
    THE PEKIOD FOLLOWING START-UP IN JULY 1973 INCLUSIVE
    TO OCTOBER 1976. THE TOTAL SCRUBBER HOURS VALUE IN-
    CLUDE OPERATION TIME WHEN ONE OR MORE OF THE MODULES
    WERE IN SERVICE. TOTAL BOILER AND UNAVAILITY VALUES
    APPLY FOR ALL THE CORRESPONDING UNITS. THE TOTAL
                                                                                            PEDCo  ENVIRONMENTAL
                                                                                                   CINCINNATI. OHIO

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                                                         PHILLIPS POWER  STATION  (CONTINUED)
MONTH
NOV.  76
DEC.  76
                          OPERATING  HOURS
                    BOILER
           12      3456
      SCRUBBER-ABSORBER
101    201    301     KOI
JAN.  77
FEB.  77
MAR.  77
                               COMMENTS
SCRUBBER AVAILABILITY INDEX INCLUDES THE TIME WHEN
ONE OR MORE MODULES WE«E AVAILABLE FOR SERVICE.
THE UTILITY REPORTS THAT BOILERS 2-6 REMAINED
COUPLED INTO THE SCRUBBING SYSTEM DURING THE REPORT
PERIOD. THE INTERIM IUCS FIXATION FACILITY WAS IN-
STALLED AND COMMENCED OPERATIONS IN DECEMBER. THE
UTILITY REPORTS THAT THE VENTURI SCRUBBERS ARE STILL
DEVELOPING LARGE AMOUNTS OF SCALE ON THE INTERNALS.
RESULTING IN TWICE NORMAL PRESSURE DROPS.  THE RECYCLE
PUMP EVALUATION HAS BEEN IN PROGRESS. APPROXIMATELY
2500 TO 2800 HOURS OF OPERATION TIME HAVE BEEN AC-
CUMULATED ON THL VARIOUS UNITS WITH NO FAILURES OR
APPRECIABLE WEAR OBSERVED. THE ADDITIONAL DEUATERING
AND REAGENT PREPARATION EQUIPMENT IS NOW BEING IN-
STALLED. THE CONTRACT HAS BEEN AWARDED TO DRAVO TO
PROVIDE THIOSORBIC LIME FOR THIS SCRUBBING SYSTEM.
ALL BOILERS HAVE BEEN HEAOEREO INTO THE SCRUBBER PLANT.
A  NUMBER OF THE UNITS HE«E DOWN FOR OVERHAUL AND REPAIR
THE INTERIM IUCS POZ-0-TEC UNIT REMAINED IN  SERVICE,
FILTERING OUT WATER ONLY. THE RECYCLE PUMP EVALUATION
IS CONTINUING. AFTER i»000 MRS. OF OPERATION, THE
CARBORUNDUM IMPELLERS AND WEAR RINGS STILL LOOK GOOD.
S02 AND PARTICULATE REMOVAL EFFICIENCIES ARE 50 * 99+*
RESPECTIVELY. INSTALLATION OF THE ADDITIONAL SILOS,
                                                                                           PEDCo  ENVIRONMENTAL
                                                                                                  CINCINNATI. OHIO

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                                                PHILLIPS POWER STATION  (CONTINUED)
MONTH
                          OPERATING HOURS
                  BOILER                  SCRUBBER-ABSORBER
                 2     3     •»     5     6     101    201    301
APR. 77

HAY  77
«»01                                  COMMENTS

      THICKENERS. AND LIME FEEDERS IS STILL IN PROGRESS. FULL

      COMPLIANCE PLANT OPERATIONS ARE SCHEDULED FOR DEC. 1977

      FULL COMPLIANCE OPERATIONS WILL INCLUDE 83* S02 REMOVAL

      FOR 2* SULFUR COAL UTILIZING THIOSORBIC LIME (6-12*MG>

      A FIXATING THE SCRUBBER HASTES WITH THE IUCS P02-0-TEC

      METHOD. THE FIXATED MATTER WILL BE HAULED AWAY TO AN

      OFF.SITE DISPOSAL AND LANDFILL. IUCS HAS BEEN AWARDED

      A 10-YEAR CONTRACT FOR THE USE OF THIS METHOD.

      THE CARBORUNDUM IMPELLORS AND WEAR RINGS CONTINUE TO

      LOOK GOOD AFTER MORE THAN 5000 HOURS OF OPERATION.

      THIOSOKBIC LIME TESTS BEGAN IN LATE MAY BUT LASTED ONLY

      ABOUT ONE WEEK. THE SCRUBBER SYSTEM WAS SHUT DOWN FOR

      3 TO if DAYS IN MAY DUE TO LEAKING IN THE WET DUCT

      HEADER THAT LEADS TO THE STACK. WHILE FIXING THE LEAK,

      INSPECTION OF OTHER COMPONENTS REVEALED THAT THE BOILER

      EXIT DAMPERS WERE ERODING. ONE 201 EXTERNAL MIST ELIMI-

      NATOR ALSO WAS SEVERLY ERODED AND PLUGGED. ONCE THE

      LEAK TO THE HEADER WAS REPAIRED, FLUE GAS FROM FOUR

      BOILERS BEGAN TO BE SCRUBBED. TWO OF THE SIX BOILERS

      ARE DOWN FOR MAINTENANCE. THE DAMPERS AND MIST ELIMINA-

      TOR REPAIRS WILL BE CORRECTED AT A SCHEDULED OUTAGE

      TIME. OVERALL SCRUBBER AVAILABILITY IS ABOUT 75 PER-

      CENT. THE INTERIM SLUDGE DISPOSAL SYSTEM STILL IS

      OPERATIONAL. THE PERMANENT SLUDGE DISPOSAL FACILITY IS

      ON SCHEDULE FOR THE DECEMBER 1977 COMPLETION DATE.
                                                                                           PEDCo  ENVIRONMENTAL
                                                                                                 CINCINNATI. OHIO 45246

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                  TABLE 5
PERFORMANCE DESCRIPTION FOR  OPERATIONAL  F6D  SYSTEMS   06/77
 IDENTIFICATION NO.

 UTILITY NAME

 UNIT NAME

 UNIT LOCATION

 UNIT RATING

 FUEL CHARACTERISTICS

 FGD VENDOR

 PROCESS

 NEW OR RETROFIT

 START UP DATE

 FGD STATUS

 EFFICIENCYt
  PARTICIPATES
  36

 KANSAS CITY POWER 4 LIGHT

 HAWTHORN NO. 3

 KANSAS CITY  MISSOURI

  140 MW

 COAL   0.5-3.5 PERCENT SULFUR

 COMBUSTION ENGINEERING

 LIME SCRUBBING

 RETROFIT

 11/72

 OPERATIONAL


 99 PERCENT
  S02
 70 PERCENT
 WATER MAKE UP
 SLUDGE DISPOSAL
 OPEN LOOP 7.0 GPM/MW
 UNSTABILIZEQ SLUDGE DISPOSED IN UNLINED POND
 UNIT COST
 OPERATIONAL
  EXPERIENCE
S19/KW CAPITAL * 2.5 MILLS/KWH OPERATING
 REFER TO THE BACKGROUND INFORMATION SECTION IN TABLE 5 OF THIS REPORT.
 THE SCRUBBER PLANT HAS BEEN CONVERTED FROM A LIMESTONE FURNACE INJECTION
 AND TAIL.END SCRUBBING STRATEGY TO A TAIL-END WET LIME SCRUBBING STHATEGr
 LIME-BASED OPERATIONS COMMENCED ON FEBRUARY 7t 1977. COMPLIANCE TESTING
 FOR KANSAS CITY PARTICULATE STANDARDS INDICATED THE NO.3 UNIT WAS WELL
 WITHIN THE 0.17 POUND REGULATION. THE 2-MODULE SCRUBBER PLANT WAS IN
 SERVICE «»08 HOURS IN APK1L (57 PERCENT OPERABILITY) AND 302 HOURS IN MAY
 (58 PERCENT OPERABILITY),
                                                                                         PEDCo  ENVIRONMENTAL
                                                                                               CINCINNATI. OHIO 45246

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                                                      BACKGROUND INFORMATION

                                                                ON

                                                       HAWTHORN NOS. 3 AND t

     THE HAWTHORN POWER STATION IS OWNED AND OPERATED BY THE KANSAS CITY POWER AND LIGHT COMPANY AND SITUATED IN A HEAVILY

INDUSTRIALIZED AREA ON THE NORTH BANK OF THE MISSOURI RIVER IN EAST KANSAS CITY. MISSOURI. THE PLANT CONTAINS FIVE COAL-FIRED

BOILERS. UNITS 1 AND 2 ARE CONSIDERED PEAK BOILERS. EACH RATED AT BO MW.  UNITS 3 AND <» ARE CYCLIC-LOAD BOILERS. EACH RATED AT

100 MW. UNIT 5 IS A BASE-LOAD BOILER RATED AT 500 MW. UNITS 1 TO H WERE PURCHASED AND PLACED IN SERVICE BETWEEN 1950 AND 1955.

UNIT NO. 5 WAS PLACED IN SERVICE IN EARLT 1970. ALL THE HAWTHORN BOILERS ARE DRY-BOTTOM PULVERIZED-COAL-FIRED UNITS DESIGNED AND

MANUFACTURED BY COMBUSTION ENGINEERING. TWO GRADES OF COAL ARE BURNED AT THE STATION. A LOW SULFUR COAL FROM THE WYOMING AREA

THAT TYPICALLY CONTAINS O.SX SULFUR AND 11 PERCENT ASH WITH A HEATING VALUE OF 9600 BTU/LB AND A HIGH SULFUR COAL FROM OKLAHOMA

THAT TYPICALLY CONTAINS s.sx SULFUR AND i* PERCENT ASH WITH A HEATING VALUE OF 11,300 BTU/LB. OF THE FIVE COAL-FIRED BOILERS

INSTALLED AT THE STATION, TWO UNITS 3 AND H HAVE BEEN RETROFITTED WITH PARTICULATE AND SULFUR DIOXIDE SCRUBBER PLANTS.

     THE ORIGINAL SCRUBBER PLANTS INSTALLED ON UNITS 3 AND «» CONSISTED OF LIMESTONE INJECTION AND TAIL-END WET SCRUBBER MODULES

SUPPLIED BY COMBUSTION ENGINEERING AND PLACED IN SERVICE NOVEMBER 1972 AND AUGUST 1972, RESPECTIVELY. A GENERAL PROCESS

DESCRIPTION OF THE PROCESS FOLLOWS* DRY LIMESTONE WAS INJECTED DIRECTLY INTO THE FURNACE BOX AND CALCINED TO LIME.  THE FURNACE-

CALCINED LIMESTONE AND BOILER FLUE GAS WERE THEN DISCHARGED TO A TAIL-END WET SCRUBBING SYSTEM CONSISTING OF TWO MARBLE-BED

ABSORBERS WHERE PARTICULATES AND SULFUR DIOXIDE WERE REMOVED FROM THE GAS STREAM. THE SPENT LIME AND OTHER SCRUBBING WASTES WERE

THEN DISCHARGED INTO A COMMON CLARIFIER TANK AND THE UNDERFLOW WAS PUMPED, UNTREATED AND UNSTABILIZED, TO AN UNLINED

DISPOSAL POND USED FOR THE DISPOSAL OF FLY ASH FROM THE OTHER BOILERS.  THE SCRUBBER PLANT INSTALLED ON EACH BOILER CONTAINED

TWO IDENTICAL MARBLE-BED ABSORBERS, EACH CAPABLE OF TREATING 500.000 ACFM OF FLUE GAS AT 300 F.  A CHEVRON-TYPE MIST

ELIMINATOR AND A FINNED-TUBE STEAM REHEATER WERE ALSO INCORPORATED IN EACH MODULE IN ADDITION TO A MIST ELIMINATOR WASH

SYSTEM  CONSISTING OF EIGHT AUTOMATICALLY-OPERATED WATER LANCES.  BY-PASSING OF THE MODULES WAS POSSIBLE THROUGH A SERIES OF

DAMPERS AND DUCTWORK AROUND EACH MODULE.

     THE ORIGINAL SCRUBBER DESIGN OF THE SYSTEM INSTALLED ON THE NO. it BOILER HAD TO BE MODIFIED SHORTLY AFTER START-UP BECAUSE

OF BOILER TUBE PLUGGING ATTRIBUTED TO THE LIMESTONE INJECTION. THE MODE OF OPERATION OF THIS SYSTEM WAS MODIFIED TO LIMESTONE

INJECTION INTO THE FLUE GAS DUCT NEAR THL INLET TO THE MARBLE-BED ABSORBER. THE SIMPLIFIED PROCESS FLOW DIAGRAMS OF THESE

ORIGINAL SCRUBBER PLANTS ARE PRESENTED IN APPENDIX B
                                                                95

                                                                                        PEDCo  ENVIRONMENTAL.
                                                                                               CINCINNATI. OHIO

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                                                      HAWTHORN UNIT NO. 3
OPERATING HOURS                                        FGO OPERA8ILITY (X)
MONTH      BOILER        MODULE 3A      MODULE 3B    MODULE A      MODULE. B                    COMMENTS
JUL. 75      584             0                          0                       PROBLEMS WITH MODULE 3A INCLUDED A LEAK IN CITY
                                                                                WATER LINE, A PLUGGED DUCT TO THE I.D. FAN.
                                                                                A MALFUNCTIONING OUTLET OA"PER FROM THE
                                                                                SCRUBBER.
                                            2<»7                       «»2        MARBLES WERE LOST FROM THE BED AND A SPRAY HEADER
                                                                                WAS BROKEN.
AUG. 75        0             0               00              0        LUST 1.0. FAN FOR HALF OF THE BOILER.  CARRYOVER
                                                                                OF JULY PROBLEMS
SEP. 75      358           247               81        69             23        OUTAGE DUE TO CLEANING AND MECHANICAL REPAIRS.
                                                                                POTS, COVERS, AND MARBLES IN THE MARBLE BED
                                                                                OF MODULE 3B WERE REPLACED.
OCT. 75      180           117             ItS         65             81        MODULE 3A OUTAGE WAS DUE LARGELY TO REPLACEMENT
                                                                                OK A RECYCLE PUMP MOTOR.  A SCHEDULED BOILER
                                                                                OVERHAUL REDUCED BOILER OPERATION HOURS.
NOV. 75        0             0               00              0        BOILER AND SCRUBBERS WERE SHUT DOWN FOR A
                                                                                SCHEDULED TRUBINE OVERHAUL.
DEC. 75        0             0               00              0        THE SYSTEM IS SCHEDULED TO 60 BACK ON-LINE IN
                                                                                JANUARY 1976.
JAN. 76        0             0               00              0        SYSTEM WAS DOWN ALL MONTH BECAUSE OF FROZEN
                                                                                EOUIPMENT AND LINES AND A MANPOWER SHORTAGE DUE
                                                                                TO A BOILER AND TURBINE OVERHAUL ON ANOTHER UNIT
                                                                                AT THIS STATION.
FEB. 76      503           140               7         37              1        SCRUBBER OUTAGES RESULTED FROM PLUGGING IN THE
                                                                                SCRUBBER BED, CAUSED BY CONVERSION FROM AN UNDER-
                                                                                BED TO OVEH-BED SPRAY SYSTEM.
                                                                96
                                                                                           PEDCo  ENVIRONMENTAL
                                                                                                  CINCINNATI. OHIO 45246

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                                                         HAWTHORN NO. 3  (CONTINUED»
OPERATING HOURS                                        FGD OPERABILITY (X)
MONTH      BOILER        MODULE 3A      MODULE 3B    MODULE A      MODULE B                    COMMENTS
MAR. 76        0             0               00              0        RECONVERSION OF MODULE 3B'S SPRAY SYSTEM ARRANGE-
                                                                                MLNT HAS BEEN COMPLETED.
APR. 76        0             0               00              0        ALSOt THE BYPASS SYSTEM HAS BEEN MODIFIED AND
                                                                                CHANGED TO A SLIDE-GATE DAMPER ARRANGEMENT.
MAY  76        0             0               00              0        THE SYSTEM WAS SHUT DOWN DURING THE MONTH DUE TO
                                                                                THE CONTINUATION OF MANPOWER SHORTAGE PROBLEMS.
                                                                                THE UTILITY DID PERFORM SOME CLEANING AND REPAIRS
                                                                                DURING THE MONTH.
JUN. 76      505             198           220         39             «»«f        THE UTILITY IS IN THE PROCESS OF MODIFYING THE
                                                                                DEMISTER WASH SYSTEM BOTH UNITS NOS. 3 AND 4.
                                                                                THE WATER LANCESt FORMERLY CONSTRUCTED OF FRPt
                                                                                ARE BEING CHANGED TO CARBON STEEL COMPONENTS IN
                                                                                OKQER TO RECTIFY LOSS OF SPRAT NOZZLES AND
                                                                                SUBSEQUENT SHATTERING OF THE LANCES,
JUL. 76                                                                         THE UTILITY IS NOW IN THE PROCESS OF CONVERTING
AUG. 76                                                                         THIS SYSTEM FROM LIMESTONE INJECTION AND TAIL END
                                                                                SCRUBBING TO A LIME SLURRY BASED SCRUBBING SYSTEM.
SEP. 76                                                                         THE SYSTEM WAS VIRTUALLY OUT OF SERVICE THE
OCT. 76                                                                         ENTIRE REPORT PERIOD.  MANPOWER COMMITMENTS WERE
                                                                                SERIOUSLY HAMPERED BY A MAJOR EXPLOSION WHICH
                                                                                OCCURRED IN THE COAL MILL PULVERIZING AREA OF
                                                                                HAWTHORN NO. 5.
NOV. 76       0               0              00              0        THE UNIT UIU NOT OPERATE DURING THE PERIOD BECAUSE
DEC. 76       0               0              0          0              0        OF THE ONGOING MAJOR MODIFICATIONS BEING IMPLE-
                                                                                MENTED TO THE SCRUBBING SYSTEM. THE SYSTEM SHOULD
                                                                                BE READY FOR OPERATION FEB.l. THE UNIT MUST UNOEH-
                                                                97
                                                                                          PEDCo  ENVIRONMENTAL
                                                                                                 CINCINNATI. OHIO

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OPERATING HOURS
MONTH      BOILER
                           HAWTHORN NO. 3 (CONTINUED)
                              FGD OPERABILITY (*)
MODULE 3A
MODULE 4 A
JAN. T7
FEB. 77
MAR. 77
0
383
482
0
337
476
0
264
411
0
86
99
0
69
85
APR. 77
HAY. 77
    foe
    302
    408
    302
57
56
57
58
GO A SERIES OF TESTS TO INSURE COMPLIANCE WITH
CITY AND FEDERAL REGULATIONS.
THE NO.3 UNIT WAS DOWN THE ENTIRE MONTH OF JANUARY
FOR COMPLETION OF MODIFICATIONS AND REPAIRS TO THE
SCRUBBERS AND BOILER. THE UNIT BECAME AVAILABLE
FOR SERVICE AND TESTING ON FEB. 7. THE UNIT'S MEA-
SURED PARTICULATE EMISSIONS AT THE SCRUBBER OUTLET
WAS 0.12 LB/MM BTU CWELL BELOW THE 0.17 LB REGS).
A BLEND OF APPROXIMATELY 2.0 PERCENT SULFUR IS
BEING FIRED IN THE BOILER. THE CONVERSION FROM
LIMESTONE TO LIME HAS BEEN GOOD. SOME INITIAL
PROBLEMS WITH PROCESS CHEMISTRY CONTROL HAVE BEEN
CORRECTED. IN ADDITION. SOME MINOR MECHANICAL
PROBLEMS IN THE FORM OF PUMP MALFUNCTIONS AND LOSS
OF SLAKING WATER PRESSURE HAVE BEEN ENCOUNTERED.
SYSTEM OPERATIONS ARE STILL CONTINUING AT OX
SOLIDS AND 100* SLOWDOWN. FRESH WATER MAKE-UP
REQUIREMENT IS APPROXIMATELY 7.0 GPM/MW.
THE SYSTEM IS NOW OPERATING WELL AT ABOUT 15-25
PERCENT SLOWDOWN.  THE PH CONTROL SYSTEM OPERA-
TIONS  HAVE BEEN EXCELLENT.  DURING MAY THE BOILER
BURNED GAS FOR 216 HOURS.  THE OPERABILITY VALUES
00 NOT INCLUDE THESE HOURS.  S02 REMOVAL EFFICIEN-
CY IS ESTIMATED AT 50-60 PERCENT FOR BOTH A AND B
                                                                98
                                                                                           PEDCo  ENVIRONMENTAL
                                                                                                  CINCINNATI. OHIO 45246

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                                            HAWTHORN wo. 3 (CONTINUED)

OPERATING HOURS                                   FGD OPERABILITY (X)
MONTH     BOILER      MODULE 3A     MODULE 3B    MODULE A     MODULE B                 COMMENTS
                                                                  SCRUBBING MODULES. ALTHOUGH ACTUAL TESTS HAVE NOT

                                                                  BEEN RUN FOR ABOUT ONE-ANO-A-HALF YEARS.  CURRENT-

                                                                  LY. BOTH MODULES ARE OPERATING SIMULTANEOUSLY.
                                                     99

                                                                           PEDCO  ENVIRONMENTAL
                                                                                CINCINNATI. OHIO 45246

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                  TABLE 5
PERFORMANCE DESCRIPTION FOR OPERATIONAL F6D SYSTEf.
 IDENTIFICATION NO.
 UTILITY NAME
 UNIT NAME
 UNIT LOCATION
 UNIT RATING
 FUEL CHARACTERISTICS
 FGO VENDOR
 PROCESS
 NEW OR RETROFIT
 START UP DATE
 FGO STATUS
 EFFICIENCYt
  PARTICULATES
                       37
                      KANSAS  CITY  POWER  «  LIGHT
                      HAWTHORN  NO.  *
                      KANSAS  CITY   MISSOURI
                       100  MW
                      COAL    0.5-3.5  PERCENT  SULFUR
                      COMBUSTION ENGINEERING
                      LIME  SCRUBBING
                      RETROFIT
                       6/72
                      OPERATIONAL

                      99 PERCENT
 S02

WATER MAKE UP

SLUDGE DISPOSAL

UNIT COST

OPERATIONAL
                       70 PERCENT
                       OPEN LOOP 7.0 GPM/MW
                       UNSTABILIZED SLUDGE DISPOSED IN UNLINED POND
                      *19/KW CAPITAL * 2.5 MILLS/KWH OPERATING
                       REFER TO THE BACKGROUND INFORMATION SECTION IN TABLE 5 OF THIS REPORT.
                       THE SCRUBBER PLANT HAS BEEN CONVERTED FROM A LIMESTONE FURNACE INJECTION
                       AND TAIL-END SCRUBBING DESIGN TO A TAIL-END WET LIME SCRUBBING SYSTEM.
                       OPERATIONS IN THE LIME SCRUBBING MODE COMMENCED ON JANUARY  1, 1977.
                       COMPLIANCE TESTING FOR KANSAS CITY PARTICULATL REGULATIONS  INDICATED  THE
                       UNIT IS MEETING THE 0.17 POUND REGULATION. THE 2-MODULE SCRUBBER PLANT
                       WAS IN SERVICE 211 HOURS IN APRIL J^a PERCENT OPERABILITY>  AND iso HOURS
                       IN HAY (5«» PERCENT OPERABILlTY).
                                                            100
                                                                                        PEDCo  ENVIRONMENTAL
                                                                                               CINCINNATI. OHIO  45246

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                                                      BACKGROUND INFORMATION
                                                                ON
                                                       HAWTHORN NOS. 3 AND "»
     THE HAWTHORN POWER STATION is OWNED AND OPERATED BY THE KANSAS CITY POWEK AND LIGHT COMPANY AND SITUATED IN A HEAVILY
INDUSTRIALIZED AREA ON THE NORTH BANK OF THE MISSOURI RIVER IN EAST KANSAS CITYt MISSOURI. THE PLANT CONTAINS FIVE COAL-FIRED
BOILERS. UNITS 1 AND 2 ARE CONSIDERED PEAK BOILERS, EACH RATED AT 80 MW.  UNITS 3 AND 
-------
                                                          HAWTHOHN NO.  "*
                  OPERATING HOURS                         FGO OPERftBILITY (X)
MONTH          BOILER    MODULE  <*A       MODULE <»B       MODULE A   MODULE B                     COMMENTS
JUL. 75         516          <*1             128             8         25         MARBLE BED PLUGGING AND STRAINER PROBLEMS ON BOTH
                                                                                MODULES.
AUG. 75                     168             212                                  LOST HALF OF BOILER DUE TO NO.  HB 1,0. FAN OUTAGE.
                                                                                BOTH FGD  MODULES WERE SHUT DOWN TO ENSURE AGAINST
                                                                                THE LOSS  OF THE ENTIRE UNIT.  NEW CHEMISTRY -
                                                                                ATTEMPTING TO RUN AT 100* SLOWDOWN AND NEAR ZERO
                                                                                PERCENT SOLIDS.  EMPHASIS ON PARTICULATE CONTROL.
                                                                                MAINTAINING PH AT 5 WITHOUT LIMESTONE INJECTION.
SEP. 75         395         206             210            52         53         SCRUBBER  MODULES WERE RETURNED  TO SERVICE ON
                                                                                SEPT. 21  AFTER REPLACEMENT OF THE ORIGINAL I.D.
                                                                                FAN ON MODULE <*B SIDE.
                                                                                NLW PROCESS DESIGN - MARBLES REMOVED FROM SCRUB-
                                                                                BER BED OF MODULE A AND REPLACED WITH A STAIN-
                                                                                LESS STEEL PERFORATED BED.  THE MARBLES WERE
                                                                                REMOVED BECAUSE OF CONTINUING OPERATIONAL DIF-
                                                                                FICULTIES.  VERY GOOD,PERFORMANCE RESULTED IN
                                                                                INCREASED AVAILABILITY AND CONTINUATION OF
                                                                                HIGH PARTICULATE REMOVAL EFFICIENCY (97 PERCENT).
OCT. 75         721         1(29            656            60         91         MINOR BOILER RESTRICTION ON THE MODULE «A SIDE
                                                                                BETWEEN THE ECONOMIZER AND THE  INLET DRAFT DUCT-
                                                                                CHEMISTRY PROCESS MODIFICATION  OF RUNNING AT 100
                                                                                PERCENT SLOWDOWN AND ZERO PERCENT SOLIDS IS STILL
                                                                                IN PROGRESS.  S02 REMOVAL EFFICIENCY IN THE 50 TO
                                                                                60 PERCENT RANGE.  KcP*L IS CONCENTRATING HEAVILY
                                                                                ON PARTICULATE EMISSION CONTROL.
                                                               102
                                                                                           PEDCo  ENVIRONMENTAL
                                                                                                  CINCINNATI. OHIO 45246

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                                                    HAWTHORN NO. U »CONTINUED!
                  OPERATING HOURS                        F60 OPERABILITY (XI
MONTH          BOILER    MODULE 4A      MODULE HB      MODULE A   MODULE B                     COMMENTS
NOV. 75         720           0            713             0         99         MODULE «»A WAS SHUT DOWN CURING THE REPORT PERIOD
                                                                                BECAUSE OF LOSS OF DRAFT THROUGH THE DUCTWORK
                                                                                FROM THE ECONOMIZER TO THE AIR PREHEATER.  THE
                                                                                REHEATER PLUGGED FREgUENTLY UNTIL THE SYSTEM WAS
                                                                                SHUT DOWN.
DEC. 75         6UO           0            103             0         16         BOILER OUTAGE OF 5 DAYS WAS DUE TO A SCHEDULED
                                                                                OVERHAUL.
JAN. 76           0           0              0             00         THE SYSTEM WAS DOWN ALL MONTH BECAUSE OF FROZEN
                                                                                EQUIPMENT AND LINES* MANPOWER WAS ASSIGNED TO A
                                                                                BOILER AND TURBINE OVERHAUL ON ANOTHER UNIT.
FEB. 76         579           0            »50             0         78         MODULE HA WAS SHUT DOWN THE ENTIRE MONTH BECAUSE
                                                                                OF CONTINUING LOSS OF DRAFT THROUGH THE DUCTWORK
                                                                                FROM THE ECONOMIZER TO THE AIR PREHEATER.  MARBLE
                                                                                BtD PLUGGING AND LOSS OF A RECYCLE PUMP OCCURRED
                                                                                ON MODULE HB.
MAR. 76         706           0             21             0          3.4       DURING THE REPORT PERIOD THE UNIT'S BYPASS SEALS
APR. 76         550         231            220            «*2         40         WERE REPLACED WITH SLIDE-GATE DAMPERS.
MAY  76         965          99             99            27         27         THE UTILITY REPORTS THE B-SIDE REHEATER IS STILL
JUN. 76         <*60         294             23            65          5         EXPERIENCING PLUGGING PROBLEMS.  ONE SECTION OF
                                                                                THE REHEAT TUBE BUNDLES HAS BEEN REMOVED IN
                                                                                ORDER TO FACILITATE CLEANING AND MAINTENANCE.
JUL. 76                                                                         CURRENTLYt THE UTILITY IS IN THE PROCESS OF
AUG. 76                                                                         MODIFYING THE SCRUBBING SYSTEM FROM A LIMESTONE
                                                                                INJECTION AND TAIL-END BASED SYSTEM TO A LIME
                                                               103
                                                                                            PEDCo  ENVIRONMENTAL
                                                                                                  CINCINNATI. OHIO

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                                                    HAWTHORN NO.  4  (CONTINUED)
MONTH          BOILER    MODULE  4A       MODULE  <»B       MODULE A     MODULE  B                    COMMENTS
                                                                                SLURRY-BASED SYSTEM.
SEP. 76                                                                         THE SYSTEM WAS OUT  OF SERVICE VIRTUALLY  THE
OCT. 76                                                                         ENTIRE REPORT PERIOD. OPERATIONS AND MANPOWER
                                                                                COMMITMENTS WERE SERIOUSLY HAMPERED BY A MAJOR
                                                                                EXPLOSION WHICH OCCURRED IN THE COAL MILL PUL-
                                                                                VERIZING AREA OF HAWTHORN NO. 5.
NOV. 76         486         442               0             91          0          THE UTILITY IS IN THE PROCESS OF CONVERTING  THE
DEC. 76          0           0                0              00          SYSTEM TO A WET-LIME  SCRUBBING SYSTEM. START-UP
                                                                                IN THE LIME SCRUBBING MODE WILL COMMENCE
                                                                                THE FIRST PART OF JANUARY.
JAN. 77         572         486              424           85         74          THE UNIT BECAME AVAILABLE FOR SERVICE IN THE LIME
FEB. 77         591         468              292           80         50          SCRUBBING MODE ON JAN.l. 1977. TESTING FOR COMPLI-
MAR. 77         539         440              525           97         82          ANCE WITH PARTICULATE CODES OCCURRED DURING  THE
                                                                                MONTH. THE 0.17 LB/MM BTU EMISSION REGULATION IS
                                                                                BEING MET BY THE NO.4 UNIT. A BLEND OF APPROXI-
                                                                                MATELY 2.OX SULFUR COAL  IS BEING BURNED IN THE
                                                                                TO REMEDY THIS. SOME  REHEAT PROBLEMS AND PLUGGING
                                                                                IN THE SUCTION OF THE RECYCLE TANK BY A RAINCOAT
                                                                                WERE ALSO REPORTED.  SYSTEM OPERATIONS ARE STILL
                                                                                CONTINUING AT 0% SOLIDS  AND 1001 SLOWDOWN. THE
                                                                                FRESH WATER MAKE-UP REQUIREMENT IS 7.0 GPM/Mw.
                                                               104
                                                                                 S/^^\
                                                                                           PEDCo  ENVIRONMENTAL
                                                                                                  CINCINNATI. OHIO 4524.6

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                                                     HAWTHORN NO. 4  (CONTINUED)

                  OPERATING HOURS                        FGD OPERABILITY (XI
MONTH          BOILER    MODULE 
-------
                  TABLE 5
PERFORMANCE DESCRIPTION FOR OPERATIONAL FGD SYSTEMS  06/77
 IDENTIFICATION NO.
 UTILITY NAME
 UNIT NAME
 UNIT LOCATION
 UNIT RATING
 FUEL CHARACTERISTICS
 FGD VENDOR
 PROCESS
 NEW OR  RETROFIT
 START UP DATE
 F6D STATUS
 EFFICIENCYi
  PARTICULATES
  38
KANSAS  CITY  POWER  &  LIGHT
LA CYGNE  NO  1
LA CYGNE  KANSAS
  820  MU
COAL  5.0  PERCENT SULFUR
BABCOCK * WILCOX
LIMESTONE SCRUBBING
NEW
  2/73
OPERATIONAL

98 PERCENT
  S02
 76  PERCENT
 WATER HAKE UP
 OPEN  LOOP  l.i»  GPM/MW
 SLUDGE DISPOSAL
 UNSTAfilLIZED SLUDGE DISPOSED IN UNLINED POND
 UNIT COST
 OPERATIONAL
  EXPERIENCE
S52/KH CAPITAL * 0.9H MILLS/KWH OPERATING
 REFER TO THE BACKGROUND INFORMATION SECTION IN TABLE 5 OF THIS REPORT.
 THE EMISSION CONTROL SYSTEM FOR THIS NEW COAL-FIRED POWER-GENERATING UNIT
 CONSISTS OF EIGHT SCRUBBER MODULES FOR FLY ASH AND S02 REMOVAL. EACH
 MODULE INCLUDES A VENTURI SCRUBBER IN SERIES WITH A 2-STAGE IMPINGEMENT
 PLATE ABSORBER.  THE SCRUBBER PLANT IS AN INTEGRAL PART OF THE POWER-
 GENERATING COMPLEX,  ALLOWING NO FLUE GAS BYPASS.  INITIAL OPERATIONS
 COMMENCED IN FEB. 1973. COMMERCIAL SERVICE WAS ATTAINED BY JUNE 1973,
 TOTAL SYSTEM AVAILABILITY FOR THE MONTH OF APRIL WAS 93 PERCENT.
                                                            106
                                                                                        PEDCo  ENVIRONMENTAL
                                                                                               CINCINNATI. OHIO

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                                                      BACKGROUND INFORMATION
                                                                ON
                                                       LA CYGNE UNIT NO. 1
     THE LA CYGNE POWER STATION OF KANSAS CITY POWER AND LIGHT COMPANY BEGAN COMMERCIAL OPERATION ON JUNE 1, 1973, AS A JOINT
PROJECT OF KANSAS 6AS AND ELECTRIC COMPANY AND KANSAS CITY POWER £ LIGHT COMPANY.  THE STATION IS LOCATED ABOUT 55 MILES SOUTH OF
KANSAS CITY, IN LINN COUNTY, KANSAS.
     ELECTRIC POWER GENERATING FACILITIES CONSIST OF ONE 820-MW COAL-FIRED BASE-LOAD BOILER WITH ASSOCIATED STEAM TURBINES AND
ELECTRIC GENERATORS.  THE PLANT HAS THREE OIL-FIRED BOILERS, USED PRIMARILY FOR STARTUP OF THE LARGE UNIT.  THEIR COMBINED
CAPACITY IS EQUIVALENT TO 26 MU.
     THE BOILER AT LA CYGNE, DESIGNED BY BABCOCK AND WILCOXt IS A DRY-BOTTOM, PULVERIZED-COAL-FIRED CYCLONE UNIT.  THE COAL
BURNED IS LOW-GRADE. SUBBlTUNlNOUS, WITH AN AS-FIRED HEATING VALUE OF 9000 TO 9700 BTU/LB AND ASH AND SULFUR CONTENTS OF 25
PERCENT AND 5 PERCENT, RESPECTIVELY.  POLLUTION CONTROL EQUIPMENT ON THIS BOILER CONSISTS OF SEVEN SCRUBBING MODULES FOR THE
CONTROL OF PARTICULATE AND SULFUR DIOXIDE. EMISSIONS.  THIS SCRUBBING SYSTEM WAS DESIGNED AND CONSTRUCTED BY BABCOCK AND WILCOX AS
AN INTEGRAL PART OF THE POWER GENERATING FACILITIES.  BYPASSING OF THE BOILER'S FLUE GAS AROUND THE FGD SYSTEM IS NOT POSSIBLE.
A PROCESS FLOW DIAGRAM OF THE LA CYGNE AIR QUALITY CONTROL SYSTEM AND RELATED MAJOR EQUIPMENT IS PRESENTED IN APPENDIX B.
PROBLEMS AND SOLUTIONS
     THE FGO INSTALLATION HAS BEEN PLAGUED WITH NUMEROUS PROBLEMS SINCE THE FIRST TRIAL OPERATION ON DECEMBER 26, 1972.  SOME OF
THESE PROBLEMS, SUCH AS VIBRATIONS OF THE INDUCED-DRAFT FANS AND THEIR SENSITIVITY TO IMBALANCE. OCCURRED EVEN BEFORE THE BOILER
WAS FIRED.  AS THESE FABRICATION PROBLEMS WERE CORRECTED AND THE FGD SYSTEM WENT INTO OPERATION, TWO OTHER TYPES OF PROBLEMS
APPEARED.   THE FIRST TYPE, ASSOCIATED WITH THE WET LIMESTONE PROCESS, INCLUDED PLUGGING OF THE DEMISTER AND STRAINERS.
THE CORROSION ASSOCIATED WITH CONDENSATION OF ACID VAPORS FROM THE GAS ON THE REHEATER TUBE BUNDLES WAS CONTROLLED BY
INJECTION OF SLIP STREAMS OF HOT AIR FROM THE BOILER'S COMBUSTION AIR HEATER INTO THE SCRUBBED FLUE GASES AT THE INLET TO THE
REHEATER UNITS.  THIS PRACTICE HAS RCDUCLD THE MAXIMUM GENERATING CAPACITY OF THE BOILER BY LIMITING.THE AIR AVAILABLE FOR COAL
COMBUSTION.
                                                               107
                                                                                          PEDCo  ENVIRONMENTAL.
                                                                                                 CINCINNATI. OHIO 45246

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LA CYGNE NO. 1 (CONTINUED)

     BECAUSE THE FGD SYSTEM INCLUDES NO SPARE MODULES AND IT CANNOT BE BYPASSED.  OUTPUT OF THE BOILER IS TOTALLY CONTROLLED BY

PERFORMANCE AND AVAILABILITY OF THE FGD MODULES.   PRESENT PROCEDURES CALL FOR CLEANING ONE MODULE EACH NIGHT ON A ROTATIONAL

SCHEDULE AND KEEPING ALL MODULES AVAILABLE DURING THE DAYTIME PEAK PERIODS.  CLEANOUTS REQUIRE THREE MEN FOR A PERIOD OF 10 TO 12

HOURS.  RECENT MODIFICATIONS BY THE UTILITY ON THE SCRUBBER INSTALLATION HAVE RESULTED IN PLANS FOR PROLONGED OPERATIONAL PERIODS,

WITH MODULES STAYING ON-LINE CONTINUOUSLY FOR PERIODS UP TO 3 WEEKS.  THIS PREVENTIVE MAINTENANCE AND CLEANOUT SCHEDULE HAS. TO

DATE, NOT YET BEEN ADOPTED.

     THE UTILITY IS CURRENTLY PLANNING ADDITIONAL SYSTEM MODIFICATIONS, INCLUDING THE INSTALLATION OF AN EIGHTH SCRUBBING MODULE

SCHEDULED TO BE IN SERVICE  THE SUMMER OF 1977.  THE ADDITIONAL MODULE IS ESTIMATED TO COST APPROXIMATELY S5.2 MILLION AND WILL

ENABLE THE PLANT TO INCREASE ITS MAXIMUM CONTlNOUS GENERATING CAPACITY FROM THE CURRENT 700-MW LEVEL TO 800 MW.  THE ORIGINAL

AIR QUALITY CONTROL SYSTEM  DESIGN ALLOTTED ADDITIONAL SPACE FOR JUST SUCH A SYSTEM EXPANSION.  OTHER SYSTEM MODIFICATIONS INCLUDE*

CHANGING THE I.Dt  FANS IN ORDER TO MINIMIZE OR ELIMINATE A FAN PARALLELING PROBLEM* CONTINUATION OF EXPERIMENTS AND MINOR CHANGES

IN ORDER TO IMPROVE SYSTEM  MECHANICAL EFFICIENCY  AND DECREASE OPERATING EXPENSES.

     ADDITIONAL DATA AND INFORMATION ON THt SUBSEUUENT SCRUBBER PLANT OPERATIONS ARE PROVIDED ON A CHRONOLOGICAL BASIS IN THE

TABLE THAT FOLLOWS.
                                                               108
                                                                                        PEDCo  ENVIRONMENTAL
                                                                                               CINCINNATI. OHIO 452-46

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                        OPERATING HISTORY

                      LA CYGNE UNIT NO. 1
PERCENT AVAILABLITT-BY MODULE
MONTH
JAN.
FEB.
MAR.
APR.
HAY
JUN.
JUL.
AU6.
SEP.
OCT.
NOV.
DEC.
JAN.
FEB.
MAR.
APR.
MAY
JUN.
JUL.
AUG.
BOILER HOURS
74
74
7*
74
7«»
7«»
74
74
74
74
74
74
75
75
75 694
75
75 683
75 667
75 590
75 630
A
49
66

67
69
92
75
90
69
90
90



82

95
88
78
75
B
32
68

70
83
84
80
90
88
71
71



96

85
85
90
88
C
44
59

75
78
83
80
73
73
60
60



90

94
84
90
87
D E
87
76
BOILER
88
85
90
81
81
76
61
61
BOILER
BOILER
BOILER
76
5 DAYS
90
85
84
78

23
52
F G
37
100

81
65
AVERAGE
50
69
SHUTDOWN
74
78
82
85
81
83
84
84
100
84
83
79
78
89
85
85
88
80
87
77
99
86
84
84
80
80
86
80
85
81
76
76
SHUTDOWN
SHUTDOWN
SHUTDOWN
93
OF
90
84
85
92
92
OPERATION
89
86
87
85
96

83
89
85
83
90

89
86
86
84
                              109
                                                                   COMMENTS
                                                    NOTE*  THE 1974 FIGURES ARE BASED UPON

                                                    ACTUAL SYSTEM OPERATION HOURS AS A FUNCTION

                                                    OF ACTUAL BOILER HOURS.  DURING REDUCED

                                                    LOAD CONDITIONS SOME OF THE MODULES WERE  NOT

                                                    REQUIRED AND THEREFORE SHUT DOWN. ALTHOUGH

                                                    THEY WERE AVAILABLE.  AVAILABILITY WAS

                                                    THEREFORE HIGHER THAN SOME OF THE POSTED

                                                    FIGURES INDICATE.  1975 FIGURES ARE BASED

                                                    UPON SYSTEM AVAILABLE HOURS AS A FUNCTION OF

                                                    HOURS IN THE PERIOD.
                                                    MODULES A ANU 0 ARE USED FOR RESEARCH TESTS.

                                                    ONE MODULE IS SHUT DOWN EACH EVENING FOR

                                                    CLEANING.
                                                          PEDCo  ENVIRONMENTAL
                                                                 CINCINNATI. OHIO 45246

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                                              F6D SYSTEM AVAILABILITY (CONTINUED)
                                                      LA CYGNE UNIT NO. 1
                                PERCENT AVAILABLITY-BY MODULE
MONTH
SEP.
OCT.
NOV.
DEC.
JAN.
FEB.
MAR.
APR.
75
75
75
75
76
76
76
76
BOILER HOURS
610
231
346
597
618
594
643

A
78
66
93
91
86
9*
92

B
84
77
90
67
85
90
90

C
84
46
60
81
91
86
88

0
85
74
93
85
72
91
93
BOILER
E
79
72
96
87
84
92
94
F G
78 74
73 65
89 94
89 84
52 84
93 95
91 91
AVERAGE
80
68
91
86
83
92
91
OVERHAUL
                                                                                                   COMMENTS
                                                                                    SYSTEM SHUTDOWN OCT. 16, 1975 OWING TO
                                                                                    PROBLEMS WITH GENERATOR AND I.D. AIR FAN.
                                                                                    SYSTEM REMAINED INOPERATIVE THROUGHOUT THE
                                                                                    HONTH.
                                                                                    AVAILABILITY FIGURES FOR OCTOBER AND
                                                                                    NOVEMBER DO NOT INCLUDE THE OUTAGE TIME FROM
                                                                                    OCTOBER 16 TO NOVEMBER 13.  BOILER OUTAGES
                                                                                    OF 80« 50. AND 11 HOURS, TOTALING 141 HOURS,
                                                                                    OCCURRED DURING DECEMBER.
                                                                                    THE SYSTEM WAS SHUT DOWN ON APRIL 6 FOR A
                                                                                    SCHEDULED BOILER, AIR PREHEATER, AND STACK
                                                                                    BREECHING OVERHAUL.  DURING THIS OUTAGE SOME
                                                                                    MAINTENANCE WAS PERFORMED ON THE SCRUBBER
                                                                                    DUCTWORK, PRIMARILY BECAUSE OF CORROSION
                                                                                    PROBLEMS.
MAY  76       436         96    92     93    96      89      95     96         94        THE SCHEDULED UNIT OUTAGE ENDED MAY 10 WHEN
                                                                                    THE SYSTEM WAS RESTARTED.  DURING THE
                                                                                    REMAINDER OF THE MONTH FOUR UNIT OUTAGES
                                                                                    WERE ENCOUNTERED. TOTALING OVER 70 HOURS.
                                                              110
                                                                                          PEDCo  ENVIRONMENTAL
                                                                                                CINCINNATI. OHIO

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                                               FGD SYSTEM AVAILABILITY  (CONTINUED*
                                                       LA CYGNE UNIT NO. 1
                                 PERCENT AVA1LABLITY-BY MODULE
MONTH     BOILER HOURS     A     8     C     D     E     F     6         AVERAGE                    COMMENTS
JUN. 76                   93    9"»     9
-------
                                          FGD SYSTEM AVAILABILITY ICONTINUED)
                                                     LA CYGNE UNIT NO. 1
                                PERCENT AVAILABILITY - BY MODULE
MONTH      BOILER  HOURS      A     B     C     0     E     F     G        AVERAGE                   COMMENTS
NOV. 76       627          95   93     94    95     94     93    94        9<»        DURING THE MONTH OF DECEMBER THE UTILITY
DEC. 76       706          87   89     81    94     94     95    91        90        CONDUCTED SOME MINOR REPAIR AND MODIFICATION
                                                                                    UORK ON THE AOCS. SPECIFICALLY A-MOOULE
                                                                                    EXPERIENCED SOME VENTURI RECYCLE PUMP
                                                                                    PROBLEMS AND THE C-MOOULE»S REHEAT STEAM
                                                                                    TUBE BUNDLES *ERE INCREASED IN NUMBER FROM
                                                                                    FOUR TO LIGHT.
JAN. 77       714          94   90     95    95     95     92    90        93        KCPiL REPORTS THAT THE 8TH MODULE HAS BEEN
FEB. 77       634          93   93     93    94     93     94    88        93        IMSTftLLED AND WILL 9E PLACED IN SERVICE SOME-
MAR. 77                   94   92     86    94     91     94    90        92        TIME DURING THE MONTH OF APRIL. THE SYSTEM
                                                                                    MOOIFICflTIONS PROSRAM IS STILL IN PROGRESS.
                                                                                    TWO CRUCIAL MODIFICATION AREAS ARE REHEAT AND
                                                                                    MIST ELIMINATION. ADDITIONAL BANKS OF STEAM
                                                                                    TUBE BUNDLES HAVE BEEN INSTALLED IN SOME
                                                                                    MODULES. THE MIST ELIMINATORS IN TWO MODULES
                                                                                    HAVE BEEN MODIFIED TO THE POINT WHERE THEY
                                                                                    HAVE BEEN OPERATING CONTINUOUSLY CLEAN. THE
                                                                                    nacs's WATER LOOP is NOW 95* CLOSED. ALSO,
                                                                                    A NEW SETTLING POND IS BEING INSTALLED AT THE
                                                                                    PLANT. THE PLANT IS STILL GENERATING 700-720
                                                                                    MW  DURING THE DAY AND 500-570 MW AT NIGHT.
                                                                                    50  F OF  REHEAT HAS BEEN DETERMINED AS THE
                                                                                    NECESSARY AMOUNT FOR THE LA CYGNE NO.l UNIT.
                                                               112
                                                                                          PEDCo  ENVIRONMENTAL-
                                                                                                 CINCINNATI. OHIO 45246

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MONTH



APR. 77



HAY  77
BOILER HOURS
                                              F6D SYSTEM AVAILABILITY (CONTINUED)




                                                      LA CTGNE UNIT NO.  1




                                PERCENT AVAILABILITY BY MODULE




                                 B     C     D     E     F      G
               COMMENTS




DURING APRIL, THE AVERAGE AVAILABILITY IN-




DEX FOR THE SEVEN MODULES WAS 92.5




PERCENT.  THE EIGHTH MODULE IS READY FOR




OPERATION AND IN FACT HAS BEEN RUN FOR TWO




DAYS.  HOWEVER, THE BOILER AND SCRUBBER




SYSTEM ULRE SHUT DOWN IN MAY DUE TO TURBINE




PROBLEMS.  THE BOILER AND EIGHT MODULES ARE




EXPECTED TO START UP ABOUT JUNE 27. WHEN IT




IS EXPECTED THAT 6gO MH WILL GO ON LINE.




THE MIST ELIMINATOR WASHING CONFIGURATION IS




BEING CHANGED TO WORK COUNTERCURRENT To THE




GAS FLOW.  ADDITIONAL TUBE BUNDLES ARE BEING




ADDED TO INCREASE THE REHEAT AREA.  THESE




CHANGES SHOULD BE TAKEN CARE OF BY THE END




OF JUNE.  THE NEW SETTLING POND IS STILL




BEING DNAUM UP.  EXCAVATION HAS NOT BEGUN.
                                                                                           PEDCo  ENVIRONMENTAL
                                                                                                  CINCINNATI. OHIO

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                  TABLE  5
PERFORMANCE DESCRIPTION  FOR  OPERATIONAL  FGD SYSTEMS   0^/77
 IDENTIFICATION  NO.

 UTILITY NAME

 UNIT NAHE

 UNIT LOCATION

 UNIT RATING

 FUEL CHARACTERISTICS

 FGD VENDOR

 PROCESS

 NEW OR  RETROFIT

 START UP DATE

 FGD STATUS

 EFFICIENCY,
  PARTICULATES
 «H


KANSAS POWER & LIGHT


LAWRENCE NO 4


LAURENCE KANSAS


 125 MH


COAL 0.5 PERCENT SULFUR


COMBUSTION ENGINEERING


LIMESTONE SCRUBBING


RETROFIT


12/66


OPERATIONAL



99 PERCENT
  S02
75 PERCENT
 WATER HAKE UP
 SLUDGE DISPOSAL
UNSTABILIZED SLUuGE DISPOSED  IN UNLINED POND
 UNIT COST
 OPERATIONAL
  EXPERIENCE
REFER TO BACKGHOUND INFORMATION SECTION IN TABLE 5 OF THIS REPORT.
THE NEW LIMESTONE FGD SYSTEM COMMENCED OPERATIONS IN EARLY JANUARY 1977-
THERE HAVE BEEN NO FORCED SCRUBBER OUTAGES SINCE START-UP.
CONTINUOUS S02 MONITORS ARE RECORDING S02 REMOVAL EFFICIENCIES
BETTER THAN 85 PERCENT, PAHTICULATE REMOVAL IS REPORTED TO
BE EXCELLENT. YIELDING NO VISIBLE PLUME. MINOR PROBLEMS HAVE
REVOLVED AROUNU MAINTAINING SOLIDS LEVELS. SEVERAL DIFFERENT
TYPES OF SLURRY PUKPS ARE BEING COMPARED UNDER OPERATING CONDITIONS.
                                                                                        PEDCo  ENVIRONMENTAL
                                                                                              CINCINNATI. OHIO

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                                                      BACKGROUND INFORMATION

                                                                ON

                                                          LAWRENCE: NO. 
-------
                 A HISTORY OF PROBLEMS WITH THE LIMESTONE INJECTION SYSTEM AT LAWRENCE NO. U

     PROBLEMS WITH THE FGO SYSTEM ON BOILER NO. «» INCLUDED BUILDUP AND PLUGGING OF THE INLET DUCT WHERE HOT GASES ENTER THE

SCRUBBERS, EROSION OF SCRUBBERS HALLS, CORROSION OF SCRUBBERS INTERNALS, BUILDUP ON 10 FAN ROTORS, AND PLUGGING OF DRAIN LINES,

MARBLE BEDS. AND OEMISTERS.  LOW S02 REMOVAL WAS CAUSED BY OVERBURNING OF THE LIMESTONE AND DROPOUT OF THE LIME WITH THE ftSH IN

THE BOTTOM OF THE SCRUBBER.

     THE SCRUBBERS WERE MODIFIED IN 1969 BY RAISING THE. OEMlSTER AND ADDING SOOT BLOWERS  IN THE INLET OUcT AND REHEATER TO REDUCE

PLUGGING.  NEW SPRAY NOZZLES WERE ALSO INSTALLED.  REHEATER PLUGGING WAS ELIMINATED BY REPLACING COPPER REHEAT COILS WITH A

CARBON STEEL UNIT HAVING WIDELY SPACED FINS.

     MAJOR MODIFICATIONS IN 1970 WERE SANDBLASTING AND COftTING OF THE INTERIOR OF THE SCRUBBERS, REPLACEMENT OF ALL INTERNAL

STEEL PIPES WITH PLASTIC AND FIBERGLASS, AND REPLACEMENT OF STAINLESS STEEL OEMISTERS WITH FIBERGLASS,  SINCE OEMlSTER PLUGGING

WAS NOT COMPLETELY ELIMINATED, THE UNIT WAS WASHED MANUALLY EVERY NIGHT TO MAINTAIN THE REQUIRED OUTPUT.

     THE MODIFICATIONS IN THE SUMMER OF 1972 ON THE TWO FSD MODULES INCLUDED ENLARGEMENT  OF THE CRYSTALLIZATION TANK, AND

INSTALLATION OF NEW PLASTIC SPRAY NOZZLES, NEW SLURRY PUMPS AND STRAINERS, AND NEW MULTIPLE MIXERS IN THE TANK.

     PROBLEMS THAT REMAINED INCLUDED CORROSION. INEFFICIENT DAMPERS. EXPANSION JOINT FAILURE, DEMISTER FOULING, RAPID EROSION

OF THE SLURRY PUMP, AND VALVE FAILURE.  OPERATION OF THE FGD SYSTEM SINCE THE FALL OF 1973 HAS BEEN THE MOST SUCCESSFUL TO DATE.

     OPERATION OF THE SCRUBBER SYSTEM ON THE WYOMING COAL HAS PROVED TO BE MORE EFFICIENT AND ECONOMICAL THAN EARLIER OPERATIONS

BECAUSE A LESSER OLGREE OF S02 REMOVAL  IS REQUIRED FOR COMPLIANCE.  THE SCRUBBtR SYSTEM IS STILL  OPERATING IN THE HIGH-SOLIDS

MODE AS AN S02 AND PARTICULATE REMOVAL  SYSTEM. NORMAL MANUAL CLEANING REQUIREMENTS HAVE BEEN REDUCED TO TWO 4-HOUR SHIFTS PER

SCRUBBER PER WEEK.

     IN 197«f THIS UNIT WAS AVAILABLE FOR OPERATION 3t3 DAYS.  FIFTY PERCENT OF THE FUEL CONSUMED  WAS COAL, 2 PERCENT FUEL OIL,

AND "»e PERCENT NATURAL GAS.  DURING Ig75 THIS UNIT WAS AVAILABLE FOR OPERATING 333 DAYS.  SIXTY-FOUR PERCENT OF THE FUEL CONSUMED

WAS COAL, 3 PERCENT FUEL OIL, AND 33 PERCENT NATURAL GAS.

     BY LATE 1976, THE ORIGINAL EMISSION CONTROL SYSTEM WAS REPLACED WITH A ROD AND SPRAY TOWER SCRUBBER FOR PARTICULATE AND

S02 REMOVAL.  INFORMATION ON THE ORIGINAL AND REPLACEMENT SYSTEM IS GIVEN IN THE FOLLOWING TABLE.
                                                               116
                                                                                           PEDCo   ENVIRONMENTAL
                                                                                                  CINCINNATI. OHIO 45246

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                 OPERATING HISTORY - NOW DEFUNCT LIMESTONE INJECTION SYSTEM - LAWRENCE NO. H
MONTH
JUL. T5

AUG. 75



SEP. 75

OCT. 75

NOV. 75

DEC. 75

JAN. 76

FEB. 76
MAR. 76

APR. 76

HAT  76

JUN. 76

JUL. 76

AUG. 76
                         OPERATING HOURS
          BOILER      MODULE A   MODULE b
                        AVAILABILITY
                      MODULE A   MODULE B
                         NOT LOGGED
NOT LOGGED
NOT LOGGED
NOT LOGGED
                                                               117
                         COMMENTS

THE FGD SYSTEM HAS OPERATED SATISFACTORILY FOR OVER A YEAR.

AVAILABILITY IS REPORTED To BE ADEQUATE FOR THE OPERATION

OF THIS STATION.  STATION LOAD IS REDUCED TO 50 PERCENT

EVERY NIGHT.  THEREFOREt ONE Op THE MODULES CAN BE TAKEN

OFF-LINE NIGHTLY FOR CLEANING OR REPAIR.  WYOMING COAL (0.5

PERCENT SULFUR) IS BEING BURNED IN THE BOILER. SOME

NATURAL GAS HAS BEEN BURNED SINCE JUNE 20.

EACH MODULE SHUT DOWN ONCE PER WEEK FOR INSPECTION AND

CLEAN-UP. NO BOILER OUTAGES OCCURRED DURING THE JULY-AUGUST

PERIOD.
PRESENT PROJECTIONS BY THE UTILITY CALL FOR THIS UNIT TO BE

AVAILABLE 330 DAYS DURING 1976.  THE FUEL CONSUMPTION WILL

BE 80 PERCENT COAL. 12 PERCENT NATURAL GAS, AND 8 PERCENT

FUEL OIL.  THE UTILITY IS REPLACING THIS SCRUBBER SYSTEM

WITH A VENTRI-ROO FOLLOWED BY A SPRAY TOWER.
                                             NO INFORMATION WAS REPORTED BY THE UTILITY FOR THE PERIOD.
                                             NO INFORMATION WAS REPORTED BY THE UTILITY FOR THE PERIOD.
                                                                                          PEDCo  ENVIRONMENTAL
                                                                                                 CINCINNATI. OHIO 45246

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MONTH


SEP. 76


OCT. 76


NOV. 76


DEC. 76
  OPERATING HISTORY




BOILER
                         OPERATING  HOURS
                      MODULE  A    MODULE B
NOW DEFUNCT LIMESTONE INJECTION SYSTEM - LAWRENCE NO. H (CONTINUED)




                                                               COMMENTS
  AVAILABILITY

MODULE. A   MODULE B
         TURBINE OVERHAUL AND REPAIR
                                       THE UTILITY REPORTS THAT THE UNIT REMAINED OUT OF SERVICE


                                       THROUGHOUT THE REPORT PERIOD AS A SCHEDULED TURBINE


                                       OVERHAUL. WHICH COMMENCED IN MID-SEPTEMBER, CONTINUED. THE


                                       NEW EMISSION CONTROL SYSTEM. CONSISTING OF


                                       A ROD SECTION AND SPRAY TOWER SCRUBBING SYSTEM, HAS


                                       BEEN INSTALLED ON THIS UNIT. INITIAL OPERATION OF THE


                                       SYSTEM WILL COMMENCE. FOLLOWING COMPLETION OF THE TURBINE


                                       OVERHAUL. THE UNIT taILL CONTINUE TO FIRE LOW SULFUR


                                       WYOMING  COAL  (0.5* SULFUR*  10,000 BTU/LB),
                                                               lie
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                               OPERATING HISTORY - WET LIMESTONE SCRUBBING Sr.^TEM - LAWRENCE NO. i»
JAN. 77      THE NEW LIMESTONE FGD SYSTEM BECAME COMMERCIALLY OPERABLE IN EARLY JANUARY 1977.  THERE HAVE BEEN NO FORCED OUTAGES
FEB. 77    AND NO DOWNTIME SINCE START-UP.  THE UTILITY REPORTS THAT BOTH pARTICULATE AND S02 REMOVALS ARE QUITE SATISFACTORY.
MAR. 77    MINOR PROBLEMS HAVE Br.EN RELATED TO MAINTAINING DESIRED SOLIDS LEVEL IN THE MAKE-UP TANK. MODIFICATION PLANS
           INCLUDE CESSATION OF SLURRY DILUTION, WHICH CURRENTLY PRECEDES THE INTRODUCTION OF THE FRESH LIMESTONE SLURKY
           INTO THE RECIRCULATION LOOP.  THE UTILITY PLANS TO PUMP THE 35-PERCENT SOLIDS SLURRY DIRECTLY FROM THE SLURRY TANK
           INTO THE RECIRC LOOP.  CURRENTLY SEVERAL DIFFERENT MAKES OF SLURRy PUMPS ARE BEING USED.  ALL ARE FUNCTIONING WELL
           so FAR* THE PUMPS HAVE NOT BEEN IN SERVICE LONG ENOUGH FOR COMPARISONS TO BE DRAWN.
APR. 77    THE SCRUBBER WAS NOT REQUIRED FOR SERVICE DURING THE REPORT PERIOD BECAUSE NATURAL GAS WAS FIRED IN THE BOILER. KP&L
MAY 77     ANTICIPATES THAT THE NATURAL GAS AVAILABILITY SHOULD LAST THROUGHOUT THE MAJORITY OF THE SUMMER, REQUIRING NO SCRUBBER
           PLANT OPERATIONS DURING THE PERIOD.
                                                               119
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                  TABLE  5
PERFORMANCE DESCRIPTION  FOR  OPERATIONAL  F6D  SYSTEMS   06/77
 IDENTIFICATION NO.
 UTILITY NAME
 UNIT NAME
 UNIT~LOCATION
 UNIT RATING
 FUEL CHARACTERISTICS
 FGD VENDOR
 PROCESS
 NEW OR RETROFIT
 START UP DATE
 FGD STATUS
 EFFICIENCY,
  PARTICULATES
KANSAS POWER & LIGHT
LAWRENCE NO 5
LAURENCE KANSAS
 *00 MW
COAL 0.5 PERCENT SULFUR
COMBUSTION ENGINEERING
LIMESTONE SCRUBBING
NEW
 6/76
OPERATIONAL

99 PERCENT
  S02
65 PERCENT
 WATER MAKE UP
 SLUDGE DISPOSAL
UNSTABILIZEO  SLUDGE DISPOSED  IN  UNLINED  POND
 UNIT COST
 OPERATIONAL
  EXPERIENCE
REFER TO THE BACKGROUND  INFORMATION  SECTION  IN  TABLE  5 OF  THIS  REPORT.
THE ORIGINAL LIMESTONE INJECTION  AND TAIL-END SCRUBBING SYSTEM  IS STILL
IN SERVICE WHILE A NLW ROD-SCRURBER  AND  SPRAY TOWER ABSORBER  SYSTEM  IS
BEING ERECTED ALONGSIDE  THE EXISTING SYSTEM. THE  NEW  SCRUBBER PLANT
INCLUDES 2 MODULES EACH  CAPABLE OF HANDLING  APPROXIMATELY  50* OF  THE  TO-
TAL BOILER FLUE GAS FLOW. THE SYSTEM DESIGNER AND SUPPLIER IS COMBUSTION
ENGINEERING. THE UNIT FIRES APPROXIMATELY  1«»0 TONS/HOUR OF LOW  SULFUR
WYOMING COAL HAVING HEAT AND SULFUR  CONTENTS OF 10,000 BTU/LB AND 0.5%.
                                                            120
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                                                      BACKGROUND INFORMATION
                                                                ON
                                                          LAURENCE NO. 5
     UNIT NO. 5 AT LAWRENCE POWFR STATION IS A CYCLIC-LOAD STEAM BOILER EQUIPPED TO BURN COAL. NATURAL GAS SUPPLEMENTED WITH OIL,
OR COMBINATIONS OF THESE FUELS.  THE BOILER, PLACED IN SERVICE IN 1971, HAS A RATED CAPACITY OF «*00 MW WHEN BURNING COAL AND

NATURAL GAS.
     THE COAL NOW BURNED AT THE LAWRENCE POWER PLANT IS A LOW-SULFUR SOUTHEAST WYOMING COAL, HAVING AN AVERAGE HEATING VALUE OF

10,000 BTU/LB AND SULFUR AND ASH CONTENTS OF 0.5 AND 11 PERCENT RESPECTIVELY.
     THE*BOILER'S ORIGINAL FGD SYSTEM WAS SUPPLIED BY COMBUSTION ENGINEERING AND PLACED IN SERVICE IN 1971. ORIGINAL EQUIPMENT
INCLUDED 6 IDENTICAL MODULES WITH A CAPACITY OF 150,000 SCFM/MODULE. EACH MODULE CONSISTS OF A SINGLE-STAGE MARBLE BED SCRUBBER
FOLLOWED BY A CHEVRON-TYPE DEMISTER AND INDIRECT STEAM REHEATER. ALL THE MODULES ARE FITTED WITH BY-PASS DUCTS AND HYDRAULIC
SEAL DAMPERS. THE PLANT INCLUDES FACILITIES FOR STORING AND MILLING LIMESTONE (COMPOSITION* 93 PERCENT CALCIUM CARBONATE, 6

PERCENT SILICA, AND i PERCENT MAGNESIUM CARBONATE).
     SPENT SLURRY FROM THE UNIT ALONG WITH THE SLURRY FROM UNIT NO. i»  IS SENT TO THREE INTERCONNECTED UNLINED SLUDGE DISPOSAL
PONDS OF 16, 26* AND H ACRES.  COOLING TOWER SLOWDOWN SUPPLIES MAKE-UP WATER TO THE POND SYSTEM. CLARIFIED POND WATER IS RECYCLED.

THE SLUDGE IS NOT TREATED FURTHER AND IS REPORTED TO SET AND SOLIDIFY  IN THE PONDS.

PROBLEMS AND SOLUTIONS
     PROBLEMS WITH THE FGD SYSTEM ON BOILER NO. 5 WERE SIMILAR PROBLEMS TO THOSE OF THE SYSTEM ON BOILER NO. <»*  LOCALIZED COR-
ROSION IN SOME EQUIPMENT, UNSATISFACTORY DAMPER OPERATION, DEMISTER FOULING, EXPANSION JOINT FAILURE, AND RAPID WEAR OF SLURRY-
RECIRCULATING PUMPS.  IN ADDITION TO THESE PROBLEMS, BOILER NO. 5 is PLAGUED WITH POOR FLUE GAS DISTRIBUTION TO THE EIGHT FGD

MODULES  WHICH, UNLIKE THE MODULES ON BOILER NO. H ARE ALL INTERCONNECTED TO A COMMON STACK.
     FGD SYSTEM AVAILABILITY WAS ADEQUATE FOR THE OPERATION OF THIS STATION. BECAUSE THE STATION LOAD WAS REDUCED TO FIFTY

PERCENT. AS  MANY AS FOUR MODULES WERE SHUT DOWN FOR CLEANING AND REPAIR EACH EVENING.
     OPERATION OF THE SCRUBBER SYSTEM ON WYOMING COAL HAS PROVED TO BE MORE EFFICIENT AND ECONOMICAL BECAUSE OF THE LESSER DEGREE

OF soa REMOVAL REQUIRED.
     IN  1971 THE UNIT WAS AVAILABLE FOR OPERATION 338 DAYS*  66 PERCENT OF THE FUEL CONSUMED WAS NATURAL GAS, 27 PERCENT COAL, AND
6 PERCENT FUEL OIL.  DURING 1975 THE UNIT WAS AVAILABLE FOR OPERATION  352 DAYS, FUEL CONSUMPTION WAS i»5 PERCENT NATURAL GAS, H2

PERCENT COAL, AND 13 PERCENT FUEL OIL.
                                                               121

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LAWRENCE UNIT NO.  5 (CONTINUED)

     KPSL« IN ORDER TO MAINTAIN  SCRUBBING OPERATIONS FOR  THIS UNIT*  IS NOW FOLLOWING A COURSE SIMILAR TO THE ONE EMPLOYED FOR THE

NO. 1 UNIT AT THIS STATION.  SPECIFICALLYt A  TWO-TRAIN VENTURI-ROD SCRUBBER AND SPRAY TOWER ABSORBER ASSEMBLY IS BEING INSTALLED

ALONGSIDE THE EXISTING MARBLE-BED  SYSTEM. THE  MARBLE-BED  UNITS WILL  REMAIN IN SERVICE UNTIL THE NEW SPRAY TOWER SYSTEM HAS BEEN

COMPLETED AND DUCTED INTO THE  BOILER  FLuE GAS  STREAM. THIS WILL OCCUR SOMETIME DURING THE COURSE OF 1978. ADDITIONAL DATA AND

INFORMATION IS PROVIDED IN THE TABLE  THAT FOLLOWS.  A FLOW DIAGRAM OF THE INJECTION SYSTEM IS PROVIDED IN APPENDIX B.
                                                               122

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MONTHS
JUL. 75

AUG. 75

SEP. 75

OCT. 75

NOV. 75

DEC. 75

JAN. 76
FEB. 76

MAR. 76

APR. 76

HAY  76

JUN. 76

JUL. 76

AUG. 76

SEP. 76

OCT. 76
  OPERATING HOURS
BOILER     FGD MODULES
                          NOT LOGGED
            NOT LOGGED
            NOT LOGGED
            NOT LOGGED
            NOT LOGGED
                  LAWRENCE NO. 5


                      COMMENTS

WYOMING COftL IS BEING BURNED IN THIS UNIT.  FGD SYSTEM AVAILABILITY IS REPORTED TO BE

ADEQUATE FOR OPERATION OF THIS STATION.  SINCE STATION LOAD IS REDUCED TO 50 PERCENT

EVERY NIGHT, AS MANY AS FOUR MODULES CAN BE SHUT DOWN FOR CLEANING AND REPAIR EACH

EVENING.

FGD UNITS HERE OFF-LINE MOST OF JUNE FOR MAJOR REBUILDING OF THE SPRAY SYSTEMS IN ALL

MODULES.  SOME OIL WAS BURNED TO ALLOW BYPASSING OF THE REPAIR.

OIL AND GAS WERE BURNED IN JULY AND AUGUST.  NO FGO OPERATION.




GAS AND OIL BURNED ON A PART-TIME BASIS DURING SEPTEMBER AND OCTOBER.  BOILER OUTAGE

WAS DUE TO INSPECTION, TURBINE REPAIR* AND REPLACEMENT OF THE SLURRY TANK SCREEN.
PROJECTIONS BY THE UTILITY FOR THIS UNIT CALL FOR 330 DAYS OF OPERATION IN 1976 WITH

FUEL CONSUMPTION BEING 60 PERCENT COAL. 25 PERCENT FUEL OIL, AND 15 PERCENT NATURAL

GAS.  LIKE UNIT H, THIS UNIT MAY BE CONVERTED To A VENTRI-RQD AND SPRAY TOHER

SCRUBBING SYSTEM.



NO INFORMATION WAS REPORTED BY THE UTILITY FOR THE PERIOD.



NO INFORMATION WAS REPORTED BY THE UTILITY FOR THE PERIOD.



NO INFORMATION WAS REPORTED BY THE UTILITY FOR THE PERIOD»



NO INFORMATION WAS REPORTED BY THE UTILITY FOR THE PERIOD.
                                                               123
                                                                                           PEDCo  ENVIRONMENTAL
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LAWRENCE N0.5CCONTINUED)
MONTHS
NOV. 76
DEC. 76
  OPERATING HOURS
BOILER     FGD MODULES
JAN. 77
FEB. 77
MAR. 77
APR. 77
HAY 77
                      COMMENTS
THE UTILITY REPORTS THAT THE INSTALLATION OF THE NEW ROD AND SPRAY TOWER SCRUBBING
SYSTEM IS NOW IN PROGRESS. THE SYSTEM WILL INCLUDE TWO SCRUBBING TRAINS. EACH
HANDLING 50 PERCENT OF THE FLUE GAS CAPACITY. FOUNDATION AND STRUCTURAL STEEL
ERECTION HAS BEEN COMPLETED. SOME OF THE BREECHING HAS BEEN INSTALLED. THE FGD
SYSTEM WILL OPERATE ON A FULLY AUTOMATED BASIS. KPSL REPORTS THAT C-E HAS
ENCOUNTERED SOME PROBLEMS WORKING OUT AND FINE-TUNING SQME QF THE LOGIC CIRCUITS.
THE BOILER FIRES NO.2 FUEL OIL IN ADDITION TO LOW SULFUR WYOMING COAL WHILE THE NEW
SCRUBBING FACILITIES ARE BEING INSTALLED. THE ORIGINAL INJECTION AND TAIL-ENO SCRUB-
BING SYSTEM IS STILL AVAILABLE FOR SERVICE AND OPERATED WHEN THE UNIT FIRES COAL,
THE SYSTEM WILL TREAT FLUE GAS RESULTING FROM THE BURNING OF LOW SULFUR
(0.5 PERCENT) WYOMING COAL.
KPSL REPORTED THAT CONSTRUCTION OF THE NEW SCRUBBING SYSTEM is STILL IN PROGRESS.
ALL FOUNDATION WORK HAS BEEN COMPLETED. ERECTION OF THE STRUCTURAL STEEL AND BREECH-
ING IS CONTINUING. THE ORIGINAL SCRUBBING SYSTEM IS STILL AVAILABLE FOR SERVICE.
THE INJECTION AND  TAIL-END SCRUBBER PLANT WAS  IN SERVICE AND OPERATED WHEN THE
BOILER FIRED COAL.  ERECTION OF THE NEW SCRUBBER PLANT is CONTINUING. THE MODULES
ARE NOW  BEING ERECTED AT  THE PLANT SITE, PARALLEL TO THE EXISTING MARBLE-BED
SYSTEM.
                                                               124
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                  TABLE s
PERFORMANCE DESCRIPTION FOR OPERATIONAL FGD SYSTEMS  06/77
 IDENTIFICATION NO.
 UTILITY NAHE
 UNIT NAME
 UNIT LOCATION
 UNIT RATING
 FUEL,CHARACTERISTICS
 FGO VENDOR
 PROCESS
 NEW OR RETROFIT
 START UP DATE
 FGD STATUS
 EFFICIENCY,
  PARTICULATES

  502
 KENTUCKY  UTILITIES
 GREEN RIVER  NOS.  1   2   AND  3
 CENTRAL CITY KENTUCKY
   6<» MU
 COAL  3.8 PERCENT SULFUR
 AMERICAN  AIR FILTER
 LIME SCRUBBING
 RETROFIT
  9/75
 OPERATIONAL

 99.7 PERCENT

 60 PERCENT GUARANTEE
 HATER MAKE UP
 SLUUGE DISPOSAL
 UNIT COST
 OPERATIONAL
  EXPERIENCE
 OPEN LOOP 1.20 GPM/MW
  STABILIZED SLUDGE DISPOSED IN  UNLINED POND
S6«/KW CAPITAL * 2.0 MILLS/KWH OPERATING
 REFER TO BACKGROUND INFORMATION SECTION IN TABLE 5 OF THIS REPORT.
 STACK REPAIRS WEKE COMPLETED DURING THE REPORT PERIOD,  AND BOILER AND
 SCRUBBER OPERATIONS RESUMED IN APRIL.  THE STACK IS NOW  LINED WITH
 PRECRETE G-ft, A REFRACTORY LINING APPLIED BY AAF.  DURING APRIL.  OPERA-
 BILITY AND RELIABILITY INDEX VALUES WERE 98*«  AND  THE AVAILABILITY  INDEX
 WAS 40X. DURING MAY, OPERABILITY AND RELIABILITY INDEX  VALUES WEK£  98X,
 AND THE AVAILABILITY INDEX VALUE WAS 99*.
                                                            125
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                                                      BACKGROUND INFORMATION
                                                                ON
                                                     GREEN KIVER POWER STATION
     THE GREEN RIVER POWER STATION IS WHOLLY OWNED AND OPERATED BT THE KENTUCKY UTILITIES COMPANY AND SITUATED ON THE GREEN RIVER,
NEAR CENTRAL CITY IN MUHLENBERG COUNTY.  KENTUCKY.  THE STATION CONSISTS OF TWO TURBINE. GENERATORS AMD FOUR COAL-FIRED BOILERS.
     AS THE RESULT OF A CONTRACT AWARDED BY KENTUCKY UTILITIES (KUI  TO AMERICAN AIR FILTErt ( AAF), A TAIL-END WET LI*E SCRUBBING
SYSTEM WAS DESIGNED AND INSTALLED ON BOILERS 1,  2, AND 3 AT THE GREEN RIVER POWER STATION.
     THE FLUE GAS UESULFURIZATION (FGD)  AND PARTICULATE. REMOVAL SYSTEM CONSISTS OF ONE SCRUBBER MODULE DESIGNED TO HANDLE A
MAXIMUM OF 360,000 ACFM OF FLUE GAS AT 300 F.  THE BLOW-THROUGH SCRUBBER MODULE CONTAINS A VARIABLE-THROAT FLOODED-ELBOW VENTURI
FOR FLY ASH REMOVAL AND A MOBILE BED CONTACTOR FOR SULFUR DIOXIDE REMOVAL.  ENTRAINED WATER DROPLETS ARE REMOVED VIA ft CENTRIFUGAL
DEMISTER BEFORE DISCHARGE TO A LOCAL STACK.  THE SLUHRY RECYCLE/DISCHARGE SYSTEM CONSISTS OF ONE COMMON ACID RESISTANT TANK WITH
TWO PARTITIONS MAKING A TOTAL OF THREE COMPARTMENTS.  COMPLETION OF CHEMICAL REACTIONS, RLCIRCULATION OF SOLUTION AND WASTES
DISCHARGE ARE CONTROLLED AND MONITORED HLRE,  MECHANICAL COLLECTORS ARE PROVIDED UPSTREAM OF THE WET SCRUBBING SYSTEM FOR PRIMARY
PARTICULATE MATTER REMOVAL.
     BOILERS 1, 2, AND 3 ARE PULVERIZED COAL-FIRED UNITS SERVICING TWO TURBINES. EACH RATED AT 32 MW (GROSS).  THE FUEL BURNED  IN
THESE UNITS IS PRIMARILY A HIGH SULFUR WESTERN KENTUCKY COAL (10,797 BTU/LB., 3.8 TO 4.0 PERCENT SULFUR, 13 TO m PERCENT ASH).
THE FGD SYSTEM CAN BE BYPASSED THROUGH A SERIES OF DUCTWORK AND GUILLOTINE DAMPERS.
     A TURNKEY CONTRACT FOR THIS PROJECT WAS AWARDED TO AAF IN JUNE 1973.  CONSTRUCTION AND INSTALLATION OF THE SYSTEM WAS COM.
PLETED BY MID-SEPTEMBER 1975.  FOLLOWING GENERAL ELECTRICAL A^D MECHANICAL DEBUGGING, WHICH INCLUDED OPERATION OF THE AGITATORS
AND PUMPS, THE UNIT WAS PUT IN SERVICE ON AIR AND WATER ONLY IN AUGUST 1975.  DURING THIS OPERATION PERIOD, THE FLOW OF GAS AND
LIQUID, OPERATION OF DAMPERS, AND SPRAY PATTERNS WERE MONITORED AND CALIBRATED.  NEXT, THE SYSTEM WAS OPERATED ON AIR AND WATER
UNDER NORMAL PROCESS CONDITIONS.  THE PURPOSE OF THIS PHA*E OF OPERATION JAS TO DETECT ANr EARLY FAILURES OF A MECHANICAL NATURE
PRIOR TO THE INITIAL FLUE GAS RUN.
     THE FLUE GAS RUN COMMENCED THE MORNING OF SEPTEMBER 13, 1975.  INITIAL OPERATION PROCEEDED ON A HALF-LOAD BASIS BECAUSE ONE
OF THE TUHBINE GENERATORS WAS OUT OF SERVICE FOR OVERHAUL AND REPAIRS.  IN ADDITION, OPERATION OF THE SCRUBBING SYSTEM WAS CON-
DUCTED ON AN OPEN-WATER-LOOP BASIS.  THIS MODE OF OPERATION (HALF LOAD, OPEN LOOP) CONTINUED INTO THE FIRST QUARTER OF 1976.   IN
MARCH.  THE SYSTEM BEGAN OPERATION AT FULL LOAD CAPACITY IN A CLOSED-WATEK-LOOP MODE.  GUARANTEED SULFUR DIOXIDE REMOVAL EFFICIENCY
IS 80 PERCENT FOR 3.8 PERCENT SULFUR COAL HAVING A HEATING VALUE EQUAL TO OR GREATER THAN 11,000 UTU/LB.
                                                               12fa
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                                              GKEEN RIVEN POWER STATION  (CONTINUED)

ADDITIONAL INFORMATION ON THE  OPERATION  OF  THIS  SYSTEM  is PRESENTED  IN THE PERFORMANCE TABLE THAT FOLLOWS. A GENERAL PROCESS

FLOW DIAGRAM IS PRESENTED IN  APPENDIX  B.
                                                              127
                                                                                          PEDCo  ENVIRONMENTAL
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                                                     GKEEN RIVER  NOS.  It  2,  AND  3
            TOTAL
PERIOD  PERIOD ( HR )
DEC. 75
AVAILABILITY = 74*
RELIABILITY = 7fl*
OPERABILITY = 65*
UTILIZATION = 35*


JAN. 76      7"*«»
AVAILABILITY = i»2*
RELIABILITY = !«**
OPERABILITY = 11*
UTILIZATION = 9*


FEB. 76      696
AVAILABILITY = 70*
RELIABILITY = <«2*
OPERABILITY = 12%
UTILIZATION = 30*
MAR. 76
AVAILABILITY = 97*
RELIABILITY = 95S
OPERABILITY = 85*
UTILIZATION = 52*
    BOILER
OPERATION 
-------
                                               GREEM RIVER NOS.  It 2»  AND  3  (CONTINUED)
            TOTAL
PERIOD  PERIOD HR

APR. 76      720

AVAILABILITY = 905

RELIABILITY = 1005

OPERABILITY = 100ft

UTILIZATION = 77*

MAY  76      7uu

AVAILABILITY = 815

RELIABILITY = 1005

OPERABILITY = 100*

UTILIZATION = 61*

JUN. 76      720

AVAILABILITY = 100k

RELIABILITY s 99*

OPERABILITY = 99*

UTILIZATION = 82%

JUL. 76      7«m

AVAILABILITY = 905

RELIABILITY = 99*

OPERABILITY = 98*

UTILIZATION = 72*

AUG. 76      7U<»

AVAILABILITY = 97*
     BOILER
OPERATION HH

       552
      MODULE
AVAILABILITY (HH)

      6U6
 MODULE CALLED
10 OPERATE (HK)

    552
 HR. K-OOULE
OPEf^ATLD

   552
        COMMENTS

THL UTILITY MADE A PRIOR COMMITMENT

T^ HUN AT 100 PERCENT OPERAHILITY

       THE MONTH OF APRIL.
       «»56
                        6Q6
                                                             U56
       597
                        720
                         596
                                                             589
       58U
                        666
                         581
                        722
                                          722
                                    THE  MAJORITY  OF  THE  TOTAL  FORCED
                                    SCRUBBER  OUTAGE  TI^E  OCCURRED
                                                                129
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                         GREEN
                                                           NOS.  1.  2.  AND 3 (CONTINUED)
            TOTAL
PERIOD  PERIOD (HR)
RELUBILITY = 97*
OPERAPILITY = 97K
UTILIZATION = 97*
SEP. 76      720
AVAILABILITY = 86*
RELIABILITY = 100*
OPERABILITY = 100*
UTILIZATION = 79*
OCT. 76
AVAILABILITY
RELIABILITY =
OPERABILITY =
UTILIZATION =
NOV. 76
AVAILABILITY
OPERABILITY :
RELIABILITY =
UTILIZATION =
DEC. 76
AVAILABILITY
OPERABILITY =
RELIABILITY =
UTILIZATION =
             = 100%
              100*
              100*
             720
             = 100*

              100*
              98*
              98*
             = 73*

              97*
              67*

              70S
    BOILER
OPERATION (HR)
     MODULE
AVAILABILITY (HR)
MODULE CALLED    HR. MODULE
TO OPERATE (HR)   OPERATED
      571
     617
   571
571
                            699
                                          699
                                                           699
     70H
                       720
                                                                70U
                                                                                  70t
                           536
                       539
                        591
                     517
                                                                                                         COMMENTS
                                                                                               BECAUSE OF VIBRATION  IN  THE  SCRUB-
                                                                                               BER BOOSTER  i.o. FAN,  NECESSITATING
                                                                                               SYSTEM SHUTDOWN ANQ REPAIR.
                                                                                               HALF-LOAD OPERATIONS  WERE  CONDUCTED
                                                                                               THROUGHOUT THE PERIOD  BECAUSE  OF
                                                                                               BEARING PROBLEMS TO ONE  OF THE TWO
                                                                                               TURBINE GENERATING UNITS.  MINOR
                                                                                               FAN PROBLEMS OCCURRED,
                                                                                               REQUIRING NO FORCED OUTAGE TIME.
              DURING THE PERIOD SOME FLUE GAS WAS
              BY-PASSED AROUND THE SYSTEM WHILE
              THE UTILITY CINDUCTED A CHECKOUT OF
              THE SCRUBBER INTERNALS AND REPLACED
              SOME OF THE PACKING SPHERES IN THE
              MOBILE BED.
                                                               130
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            TOTAL
PERIOD  PERIOD (HR)
JAN. 77    7"»"4
AVAILABILITY = 9<*X
OPERABILITY = 9«*
RELIABILITY = 9<*X
UTILIZATION = 9<*X
FEB. 77    672
AVAILABILITY = 36*
RELIABILITY = 91%
OPERABILITY = 91«
UTILIZATION = 36X
MAR. 77      0
ALL INDEX VALUES = OX
    BOILER
OPERATION 
-------
            TOTAL


PERIOD  PERIOD (HR)


MAY  77    7<*<»


AVAILABILITY = 99*


RELIABILITY = 98*


OPERABILITY s 98*


UTILIZATION = 69X
    BOILER


OPERATION (HK)


    527
       GREEN RIVER NOS. It 2. AND 3 (CONTINUED)


     MODULE          MODULE CALLED     HR. MODULE


AVAILABILITY < HR )     TO OPERATE (HR)    OPERATED


     736                  527            513
          COMMENTS

THE STACK WAS REPAIRED FIRST BY

WELDING A BACKUP METAL PLATE TO THE

PORTIONS OF THE STACK WHE^E PITTING

OCCURRED.  THEN Twf; ENTIRE STACK

WAS LINED WITH ^EFHACTOKY COATING

CALLED PPECRETE G-S BY AAF.  STACK

REPAlKS WEKE COMPLETED MARCH 7.
                                                               132
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                  TABLE 5
PERFORMANCE DESCRIPTION FOR OPERATIONAL FGD SYSTEMS  06/77
 IDENTIFICATION NO.


 UTILITY NAME


 UNIT NAME


 UNIT LOCATION


 UNIT RATING


 FUEL CHARACTERISTICS


 FGD VENDOR


 PROCESS


 NEW OR RETROFIT


 START UP DATE


 FGD STATUS


 EFFICIENCY*

  PARTICULATES
 LOUISVILLE GAS X ELECTRIC


 CANE RUN NO t


 LOUISVILLE KENTUCKY


  178 MW


 COAL 3.5 - H.O PERCENT SULFUR


 AMERICAN AIR FILTER


 LIME SCRUBBING


 RETROFIT


  8/76


 OPERATIONAL



 99 PERCENT GUARANTEE
  S02
 90 PERCENT GUARANTEE
 WATER MAKE UP
 SLUDGE DISPOSAL
  STABILIZED SLUDGE DISPOSED IN  UNLINED POND
 UNIT COST
S50/KW (INCLUDING LIME AND SLUDGE DISPOSAL FACILITIES)
 OPERATIONAL
  EXPERIENCE
 REFER TO THE BACKGROUND INFORMATION SECTION IN TABLE 5 OF THIS REPORT.
 SCRUBBER OPERATIONS WERE TERMINATED APRIL 18 FOR  THE IMPLEMATiON OF
 SEVERAL MODIFICATIONS TO THE FGD SYSTEM.  A CHEVRON-TyPE MIST ELIMINATOR
 WILL BE INSTALLED*  A NEW SPRAY HEADER WILL INCREASE L/Gi REHEAT WILL
 BE ADDED AND THE CARBOLINE DUCT LINING WILL BE REPLACED WITH
 PLASTITE i»005 »BY GENERAL COATINGS).  THE MODIFICATIONS ARE EXPECTED To
 BE COMPLETE BY JULY 5.
                                                            133
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                                                      BACKGROUND INFORMATION

                                                                ON

                                                          CANE RUN NO.  
-------
PERIOD   HOURS   BOILER (HR)  SCRUBBERS IHR)
AUG. 76   7«C*       740          666
                     FGD SYSTEM PERFORMANCE
                      CANE RUN UNIT NO. 
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PERIOD   HOURS   BOILER (HR)   SCRUBBERS (HR)



NOV. 76   730
DEC. 76   7Ut


JAN. 77   7U<»       0             0
                                    FGD SYSTEM PERFORMANCE
                                     CAME RUN UNIT NO. <»
                              PERFORMANCE FACTORS <*)
                             OPERABILITY   UTILIZATION
                                 95
                                 90
FEB. 77   672
MAR. 77   7«»H
  132          356
 •AFTER       (AFTER
RESTART!     RESTART)
  83*
 (AFTER
RESTART)
  83%
 (AFTER
RESTART)
APR. 77
MAY  77
                              COMMENTS
OF THE SYSTEM, AS A FUNCTION OF SERVICE TIME VERSUS
OUTAGE TIME. HAS BEEN VERY GOOD.
THE SYSTEM INCURRED NO MAJOR PROBLEMS OR UPSETS
DURING THE REPORT PERIOD. CARBIDE LIME SLURRY IS
EMPLOYED »S THE SULFUR DIOXIDE ABSORBENT.
DURING JAN.l - JAN.11, THE SCRUBBER WAS UTILIZED 95
PERCENT OF THE TIME. THEN THE GREEN RIVER BECAME IM-
PASSABLE DUE TO ICE FORMATION AND THIS CAUSED THE
CESSATION OF BARGE DELIVERIES OF LIME.
DURING FEBRUARY, THE SCRUBBER WAS ONLY OPERATED FOR
TWO <»-HOUR PERIODS TO PREVENT TOTAL FREEZE-UP.
IN MARCH, THE SCRUBBER CAME BACK ON-LINE AT 10 AM.
ON MARCH IHTH, AND HAS RUN CONTINUOUSLY THROUGH
THE END OF THE PERIOD. FROM THE IfTH THROUGH THE END
OF THE MONTH, THERE WAS ONE PERIOD OF SCRUBBER BY-PASS,
WHEN DC SUPPLY TO THE BY-PASS HAD To BE REPAIRED-
THE SCRUBBER SYSTEM RAN FOR THE FIRST 18 DAYS IN APRIL,
WITH A RELIABILITY OF 95*.  FROM THAT TIME  (APRIL le>
THROUGH AN EXPECTED DATE OF JULY 12, THE SCRUBBER
SYSTEM WILL BE DOWN FOR THE FOLLOWING MODIFICATIONS*
1.  TO REMOVE DEMISTER AND REPLACE WITH CHEVRON UNITS.
                                                               136
                                                                                           PEDCo  ENVIRONMENTAL
                                                                                                  CINCINNATI. OHIO 45246

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PERIOD   HOURS   BOILER I MR I   SZRUBBER INK)
      FGD SYSTEM PERFORMANCE
       CANE RUN UNIT NO. <*
PERFORMANCE FACTORS(X)
OPERABILITY   UTILIZATION
                                                          COMMENTS
                            2.  TO INCREASE L/G BY ADDING A NEW SPRAY HEADER.
                            3.  TO ADD DIRECT. OIL-FIRED REHEAT, AND
                            4.  TO REPLACE THE LINING IN THE SYSTEM FROM
                                THE DEMISTEH THROUGH THE STACK WITH PLASTITE «*oos
                                TO BE INSTALLED BY GENERAL COATINGS. (THE ORIGINAL
                                LINING WAS BUBBLING. BUT HAD NOT YET FAILED* FAIL-
                                URE SEEMED IMMINENT WITHIN 1-5 MONTHS.)
                                                               137
                                                                                          PEDCo   ENVIRONMENTAL.
                                                                                                 CINCINNATI. OHIO 45246

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                  TABLE  5
PERFORMANCE DESCRIPTION  FOR  OPERATIONAL  F6D  SYSTEMS   06/77
 IDENTIFICATION  NO.

 UTILITY NAME

 UNIT NAME

 UNIT LOCATION

 UNIT RATING

 FUEL CHARACTERISTICS

 FGD VENDOR

 PROCESS

 NEW OR  RETROFIT


 START UP DATE

 FGD STATUS

 EFFICIENCY,
  PARTICULATES
  51


 LOUISVILLE GAS * ELECTRIC


 PADDYS RUN NO fa


 LOUISVILLE KENTUCKY


   65 MW


 COAL 3.5 - 
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                                                      BACKGROUND INFORMATION

                                                                ON

                                                        PADDY'S RUN NO. 6

     PADDY'S RUN POWER STATION J3 LOCATED IN LOUISVILLE, KENTUCKY.  THE PLANT HAS SIX ELECTRIC POWER GENERATING UNITS WITH A TOTAL

RATED CAPACITY OF 320 MW. UNIT NO. 6 IS RETROFITTED WITH A CARBIDE LIME-BASE FGD SYSTEM.

     UNIT NO. 6 IS A PEAK LOAD COAL-FIRED BOILER. MANUFACTURED BY FOSTER WHEELER AND INSTALLED IN 1950.  THIS UNIT FIRES COAL WITH

A GROSS HEATING VALUE OF 11.500 BTU/LB AND AVERAGE SULFUR AND ASH CONTENTS OF 3.7 PERCENT AND 13 PERCENT, RESPECTIVELY.

     THE FGD SYSTEM CONSISTS OF TWO MODULES.  EACH HANDLES 175,000 ACFn OF 350 F FLUE GAS.  EACH MODULE IS MADE UP OF TWO STAGES

OF 3-INCH MARBLE BEOS, FOLLOWED BY A TWO-STAGE CHEVRON-TYPE DEMISTER.  THE GAS IS REHEATED BY DIRECT COMBUSTION OF NATURAL GAS.

SCRUBBING SYSTEM PROVIDING PRIMARY CONTROL OF PARTICIPATE EMISSIONS. THIS UNIT OPERATES WITH A 99.1 PERCENT PARTICULATE REMOVAL

EFFICIENCY. PARTICULATE LOADING AT THE ESP OUTLET IS 0.05 GR/SCF.  A PROCESS FLOW DIAGRAM IS PROVIDED IN APPENDIX B.

     THE SYSTEM UTILIZES A SLURRY OF CARBIDE LIME AS THE SULFUR DIOXIDE ABSORBENT.  THE CARBIDE LIME, A WASTE BY-PRODUCT OBTAINED

FROM A NEARBY ACETYLENE MANUFACTURING PLANT CONTAINS 90 TO 92 PERCENT CALCIUM HYDROXIDE, 2.0 TO 2.5 PERCENT SILICA, 3.0 TO 8.0

PERCENT CALCIUM CARBONATE, AND 0.1 PERCENT MAGNESIUM OXIDE.

     THE UNIT OPERATES IN A CLOSED-LOOP MODE*  THE SULFUR.DIOXIDE IS ABSORBED IN THE MARBLE BED BY A SLURRY OF CALCIUM SULFITE TO

FORM A MIXTURE OF CALCIUM SULFITE/BISULFITE.  EFFLUENT FROM THE MARBLE-BED TOWER is CONVERTED IN THE REACTION TANK TO CALCIUM

SULFITE BY THE ADDITION OF CALCIUM HYDROXIDE.  HALF OF THE REACTION TANK EFFLUENT IS RETURNED TO THE ABSORBER TOWERS WHILE THE

OTHER HALF is FED TO A CLARIFIER TANK.  THE CALCIUM SULFITE CRYSTALS PRECIPITATE WITH THE AID OF A FLOCCULANT, WHICH is ADDED AT

THE RATE OF » TO 7 PPM.  THE OVERFLOW is RETURNED TO THE REACTION TANK.  THE UNDERFLOW. CONTAINING 22 TO 2* PERCENT SOLIDS, is

STABILIZED BY MIXING IT WITH LIME.  APPROXIMATELY 60 TO 100 POUNDS OF LIME ARE USED PER TON OF DRV SOLIDS OF SLUDGE.  THE FIXED

SLUDGE IS TRANSPORTED BY TRUCKS TO A 10-ACRE OFF-SITE LANDFILL AREA.
                                                               139

                                                                                           PEDCo  ENVIRONMENTAL
                                                                                                 CINCINNATI. OHIO 45246

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MONTH
APR. 73

MAY  73



JUN. 73

JUL. 73



AUG. 73
SEP. 73

OCT. 73
NOV. 73
DEC. 73
JAN. 74
THROUGH
JUL. 74
  OPERABILITY Ik)
MODULE A  MODULE B
  18        56
  11
  21
  53
  85

  49
  35
  44
   0
 21
 64
 72

 94
100
 78
  0
                   FGD SYSTEM OPERABILITY
                     PADDY'S RUN NO. 6
                                   COMMENTS
MODULES WERE OPERATED ONE AT A TIME. WITH FREQUENT SHUTDOWNS FOR INSPECTION OF EQUIPMENT AND
MINOR REPAIRS.
SINGLE-MODULE OPERATION CONTINUED THROUGH MAY 19, WHEN THE UNIT WAS SHUT DOWN FOR MODIFICA-
TIONS.  THE MOST SIGNIFICANT MODIFICATION WAS INSTALLATION OF EQUIPMENT FOR INJECTION OF A
FLOCCULATING AGENT INTO THE CLARIFIER TANK.
OPERATION WAS INTERMITTENT FROM JUNE 19 TO JULY n BECAUSE OF MECHANICAL PROBLEMS WITH THE
SLURRY PUMPS.
DURING A SCHEDULED OUTAGE FROM JULY 12 THROUGH AUGUST 1« SEVERAL REPAIRS WERE MADE TO THE LIME
SLURRY MAKEUP SYSTEM.  A DISINTEGRATOR UNIT WAS INSTALLED TO REDUCE PLUGGING OF STRAINERS AND
SLURRY CONTROL VALVES.
THE OPERATION WAS CONTINUOUS FROM AUGUST Z To AUGUST 18 EXCEPT FOR A BRIEF SHUTDOWN DUE TO A
BOILER-RELATED PROBLEM.  FROM AUGUST 19 TO SEPTEMBER 5. THE SYSTEM WAS SHUT DOWN TO REPLACE THE
CLARIFIER'S UNDERFLOW LINE WITH ONE OF LARGER DIAMETER AND TO INSTALL ADDITIONAL PUMP CAPACITY
IN THE CLARIFIER'S OVERFLOW SYSTEM.
THE UNIT OPERATED CONTINUOUSLY BETWEEN SEPTEMBER 6 AND SEPTEMBER 20 EXCEPT FOR A 7-HOUR SHUT-
DOWN TO REPAIR A MARBLE BED SUPPORT PLATE.  THE UNIT WAS SHUT DOWN THE REMAINDER OF THE MONTH
THE FGD SYSTEM REMAINED IN SERVICE TO DEC. 20 AFTER WHICH THE BOILER AND THE SCRUBBER MODULES
WERE SHUT DOWN BECAUSE OF NO DEMAND*(THIS IS A PEAKING-LOAD BOILER).

BOILER SHUT DOWN BECAUSE OF NO DEMAND.*
                                                               140
                                                                                           PEDCo  ENVIRONMENTAL
                                                                                                 CINCINNATI. OHIO 45246

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MONTH
AUG. 7H
SEP. 7«»
OCT. 7*
NOV. 7<»
THROUGH
AUG. 75
SEP. 75
OCT. 75
NOV. 75
DEC. 75


JAN. 76
FEB. 76
  OPERABILITY <*)
MODULE A  MODULE B
  50
   0
 100
 NO DEMAND
 77
  0
100
 100
 100
 100
  90
100
100
100
 90
 100       100
 NO DEMAND
                   FGD SrSTEM OPERABILITY
                     PADDY'S RUN NO. 6

                    COMMENTS (CONTINUED)
UNIT HAS BEEN ON AND OFF FREQUENTLY DUE TO FLUCTUATION IN POWER DEMAND.
BOILER DOWN BECAUSE OF NO DEMAND.
BOILER TURNED ON SPECIFICALLY TO PERFORM LIMESTONE TESTS ON FGD SYSTEM.
BOILER AND FGO SYSTEM OPERATIONAL ALL OF SEPTEMBER AND FIRST TWO WEEKS IN OCTOBER.  SYSTEM
OUTAGE DURING THE LAST TWO WEEKS OF OCTOBER WAS DUE PRIMARILY TO BREECHING IN THE BOILER
SECTION.  OPERABILITY FOR BOTH MODULES DURING THE OPERATIONAL PERIOD WAS 100 PERCENT (BASED
UPON LGSE'S PEAK LOAD DETERMINATION).  S02 REMOVAL WAS REPORTED To BE OVER 98 PERCENT.
BOILER AND SCRUBBER SYSTEM RAN MOST OF THE REPORT PERIOD ON A MONDAY-THROUGH-FRIDAY BASIS.  TWO
MINOR OUTAGES IN DECEMBER WERE DUE TO MALFUNCTION AND REPAIR OF THE DUAL STRAINER SWITCH SHAFT
IN THE BOTTOM OF THE SCRUBBER MODULE.
S02 REMOVAL EFFICIENCY WAS REPORTED TO BE 99 PERCENT DURING JANUARY.  THE SYSTEM WAS SHUT DOWN
IN EARLY FEBRUARY IN PREPARATION FOR AN EPA SCRUBBER/SLUDGE STUDY SCHEDULED FOR JUNE OR JULY.
THE SCRUBBER WILL NOT BE OPERATED UNTIL THE START OF THE STUDY PROGRAM UNLESS THE BOILER IS
REQUIRED FOR PEAKING POWER DEMANDS.  HIGHLIGHTS OF THE SCRUBBER/SLUDGE STUDY PROGRAM ARE AS
FOLLOWS*
     6 MONTH DURATION.
     ONE SCHEDULED SHUTDOWN FOR TEST MODIFICATIONS.
                                                                                          PEDCo  ENVIRONMENTAL
                                                                                                 CINCINNATI. OHIO 45246

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MONTH
MAR. 76

APR. 76

MAY  76

JUN. 76
JUL. 76

AUG. 76



SEP. 76

OCT. 76
NOV. 76

DEC. 76
  OPERABILITY (X)
MODULE A  MODULE B
   NO DEMAND

   NO DEMAND

100        100

100        100
100

100
100

100
   NO DEMAND
 99

 99
 99

 99
                   FGO SYSTEM OPERABILITY

                     PADDY'S RUN NO. 6


                    COMMENTS (CONTINUED)

     DELIBERATE HIGH CHLORIDE CONCENTRATION OPERATION.

     MGO INNOCULATION.

     EXTENSIVE SLUDGE STUDY*  FIXATION. LEACHATES. SEASONAL VARIATIONS.

THE UNIT DID NOT OPERATE DURING THE REPORT PERIOD IN ANTICIPATION OF THE EPA SCRUBBER/SLUDGE

STUDY.  THE UTILITY IS NOW COMPLETING SYSTEM MODIFICATIONS FOR THE OPERATION OF THE TEST

PROGRAM.  THIS PEAK LOAD UNIT WAS OPERATED PART OF THE TIME DURING THE REPORT PERIOD (APPROXI-

MATELY 2 WEEKS IN MAY AND 2 WEEKS IN JUNE).  THE SCRUBBER WAS AVAILABLE TO THE BOILER 100

PERCENT OF THE TIME.  S02 REMOVAL EFFICIENCY WAS 98 TO 99 PERCENT DURING THIS OPERATING SEG-

MENT.  THE EPA-SPONSORED SCRUBBER/SLUDGE STUDY IS NOW SCHEDULED TO COMMENCE SEPTEMBER 1, 1976.

THE UNIT WAS OPERATIONAL PART OF THE TIME DURING THE JULY-AUGUST PERIOD.  THE SCRUBBING SYSTEM

WAS AVAILABLE TO THE BOILER ON A 100 PERCENT BASIS.  NO MAJOR SCRUBBER-RELATED PROBLEMS WERE

ENCOUNTERED.

THE UNIT DID NOT OPERATE THROUGHOUT SEPTEMBER AND THE FIRST 3 WEEKS OF OCTOBER.

THE EPA-FUNDED SCRUBBER/SLUDGE STUDY PROGRAM COMMENCED OCTOBER 25.  THE INITIAL PHASE OF

THE PROGRAM CALLS FOR OPERATIONS TO PROCEED FOR A 20 TO 30-DAY PERIOD WITH CARBIDE LIME

SCRUBBING ABSORBENT.  FOLLOWING COMPLETION OF THIS RUN. THE UNIT WILL BE SHUT DOWN AND

MODIFICATIONS WILL BE INCORPORATED INTO THE SYSTEM FOR OPERATION WITH COMMERCIAL GRADE  (HIGH

CALCIUM) LIME.

THE UNIT WAS IN SERVICE DURING THE REPORT PERIOD. THE SCRUBBING SYSTEM OPERATED 99.5 PERCENT

OF THE TIME THE BOILER WAS IN SERVICE. CARBIDE LIME WAS EMPLOYED AS THE S02 ABSORBENT.  THE

HIGH CALCIUM (VIRGIN) LIME RUN, SCHEDULED AS PART OF THE SCRUBBER/SLUDGE STUDY, WILL COMMENCE

ON MARCH 1. 1977.
                                                               112
                                                                                           PEDCo  ENVIRONMENTAL
                                                                                                  CINCINNATI. OHIO  45246

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                                                      FGD SYSTEM OPERABILITY

                                                        PADDY'S RUN NO. b

               OPERABILITY (X)

MONTH        MODULE A  MODULE E                        COMMENTS (CONTINUED)

JAN. 77                            BECAUSE OF SEVERE WEATHER CONDITIONS. THERE WERE NO BOILER OPERATIONS AND NO SCRUBBER

FEB. 77                            OPERATIONS  UNTIL MARCH 15, 1977.

MAR. 77         99        99       BOILER AND SCRUBBER RESTART OCCURRED ON MARCH 15 AND OPERATION WAS CONTINUOUS THROUGH THE
               (AFTER RESTART)
                                   END OF MARCH.  THERE WERE NO PROBLEMS AND ONLY ONE HOUR OF SCRUBBER DOWNTIME.



APR. 77                            A HIGH-CALCIUM LIME RUN. WITH MAGNESIUM HYDROXIDE ADDITION* WAS STARTED IN MARCH AND RAN

MAY  77                            THROU6H MID-APRIL.  THE SCRUBBER AVAILABILITY WAS ABOUT 9S-98X (ONTIME VERSUS OFFTIMEU  S02

                                   REMOVALS OF GREATER THAN 99 PERCENT WERE CONSISTENTLY OBTAINED DURING THESE TESTS.

                                   FROM MID-APRIL UNTIL THE PRESENT, THE SCRUBBERS HAVE BEEN BYPASSED, NOT BECAUSE OF NON-

                                   AVAILABILITY, BUT BECAUSE THE BOILER LOAD HAS CAUSED THE SCRUBBER CREW TO BE TRANSFERRED TO

                                   BOILER OPERATIONS.  NON-AVAILABILITY WAS THUS CAUSED BY A LACK OF MANPOWER TO RUN THE SYSTEMS.

                                   SCRUBBER OPERATIONS ARE EXPECTED TO RESTART IN MID-JUNE, ONCE AGAIN UTILIZING A HIGH-CALCIUM

                                   LIME ADDITIVE.
                                                                                          PEDCo  ENVIRONMENTAL
                                                                                                 CINCINNATI. OHIO 45246

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                  TABLE:  s
PERFORMANCE DESCRIPTION  FOR  OPERATIONAL  FGO  SYSTEMS   oe/77
 IDENTIFICATION NO.
 UTILITY NAME
 UNIT NAME
 UNIT LOCATION
 UNIT RATING
 FUEL CHARACTERISTICS
 FGO VENDOR
 PROCESS
 NEW OR  RETROFIT
 START UP DATE
 F6D STATUS
 EFFICIENCY,
  PARTICULATES
  5«f
 MONTANA POWER CO.
 COLSTRIP NO 1
 COLSTRIP MONTANA
  360 MW
 COAL 0.8 PERCENT SULFUR
 ADL/COMBUSTION EQUIP ASSOCIATE
 LIME/ALKALINE FLYASH SCRUBBING
 NEW
 10/75
 OPERATIONAL

 99 PERCENT
  S02
 60 PERCENT
 WATER  MAKE  UP
 SLUDGE  DISPOSAL
 CLOSED LOOP
 UNSTABILIZED SLUDGE DISPOSED IN UNLINED POND
 UNIT  COST
 OPERATIONAL
  EXPERIENCE
S50/KW CAPITAL
 THE COLSTRIP PLANT IS A MINE MOUTH INSTALLATION. THE FGD SYSTEM STARTED
 UP IN LATE 1975 AND PROCEEDED THROUGH A SHAKEDOWN AND DEBUGGING OPEK-
 ATION PHASE. THE UNIT HAS BEEN OPERATING AT FULL COMERCIAL CAPACITY.
 THE SCRUBBING SYSTEM DESIGN INCORPORATES VENTURI WET SCRUBBERS FOR
 PARTICULATE AND SULFUR DIOXIDE REMOVAL. FLUE GAS CANNOT BE BY-PASSED
 AROUND THE SCRUBBING SYSTEM. INFORMATION AND OPERATING DATA WERE NOT
 MADE AVAILABLE BY THE UTILITY DURING THE REPORT PERIOD.
                                                                                         PEDCo  ENVIRONMENTAL
                                                                                               CINCINNATI. OHIO 45246

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                  TABLE 5
PERFORMANCE DESCRIPTION FOH OPERATIONAL FGD SYSTEMS  06/77
 IDENTIFICATION NO.

 UTILITY NAME

 UNIT NAME

 UNIT LOCATION

 UNIT RATING

 FUEL CHARACTERISTICS

 FGD VENDOR

 PROCESS

 NEW OK RETROFIT

 START UP DATE

 FGD STATUS

 EFFICIENCY*
  PARTICULATES
  55

 MONTANA POWER CO.

 COLSTRIP NO 2

 COLSTRIP MONTANA

  360 MW

 COAL 0.0 PLRCENT SULFUR

 ADL/COMBUSTION EQUIP ASSOCIATE

 LIME/ALKALINE FLYASH SCRUBBING

 NEW

  7/76

 OPERATIONAL


 99 PERCENT
  S02
 60 PERCENT
 WATER MAKE UP
 SLUDGE DISPOSAL
 UNIT COST
 OPERATIONAL
  EXPERIENCE
 CLOSED LOOP
 UNSTABILIZED SLUDGE DISPOSED IN UNLINED POND
S50/KW CAPITAL
 THE COLSTRIP PLANT IS A MINE MOUTH FACILITY.  INITIAL OPERATION OF THE
 SCRUBBING SYSTLM COMMENCED IN JULY 1976.  THIS UNIT IS IDENTICAL TO
 THE NO.l SYSTEfl DESIGN IN THAT THREE SCRUBBER MODULES ARE INSTALLED FOR
 PARTICULATE AND SULFUR DIOXIDE REMOVAL.  FLUE  GAS CANNOT BE BY.PASSED
 AROUND THE SCRUBBING SYSTEM. INFORMATION AND  OPERATING DATA WERE NOT
 MADE AVAILABLE BY THE UTILITY DURING THE REPORT PERIOD.
                                                            145
                                                                                        PEDCo  ENVIRONMENTAL
                                                                                               CINCINNATI. OHIO 45246

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                                                      BACKGROUND INFORMATION
                                                                ON
                                                      COLSTR1P UNITS  1  AND 2
     THE COLSTRIP POWER STATION OF THE MONTANA POWER COMPANY IS LOCATED NEAR COLSTRIP,  MONTANA,  APPROXIMATELY 100 MILES EAST OF
BILLINGS, MONTANA.  THE STATION CONTAINS TWO NEW 360-MW COAL-FIRED POWER-GENERATING UNITS.   AT  THE PRESENT TIME,  THE UTILITY IS
PLANNING THE ADDITION OF TWO MORE 700-MW COAL-FIRED POWER-GENERATING  UNITS AT THE STATION.  THIS  MINE MOUTH PLANT  FIRES LOW-SULFUR,
LOW HEAT CONTENT COLSTRIP COALi PRODUCING A FLUE GAS CONTAINING UP TO 6 GR/SCFD PARTICULATE AND  UP To 1000 PPM SuLFuR DIOXIDE.
THE GENERAL CHARACTERISTICS OF THIS COAL ARE*  HEATING VALUE (AS FIRED). 8555 BTU/LB.*  SULFUR  CONTENT,  0.77 PERCENT* ASH CONTENT,
8.59 PERCENT* MOISTURE CONTENT, 23.87 PERCENT.
     IN ORDER TO MEET AIR POLLUTION EMISSION STANDARDS OF 400 PPM FOR SULFUR DIOXIDE (1.0 LB/MM  BTU) AND 0.03 GR/SCFO FOR PARTIC-
ULATES.  THE BOILERS ARE EQUIPPED WITH SCRUBBER PLANTS FOR THE CONTROL  OF PARTICULATES  AND SULFUR DIOXIDE.  THE SYSTEMS INSTALLED
ON UNITS 1 AND 2 WERE DESIGNED AND SUPPLIED BY COMBUSTION EOUIPMENT ASSOCIATES CCEA) AND AUTHUR  0. LITTLE (ADL).   THE PROCESS
INSTALLED UTILIZES THE HIGH ALKALINITY OF THE FLY ASH (APPROXIMATELY  20 PERCENT CALCIUM OXIDE)  FOR THE REMOVAL OF SULFUR DIOXIDE
AND SUPPLEMENTAL LIME SLURRY FOR PH AND SCALE CONTROL.  DESIGN PARTICULATE AND SULFUK DIOXIDE  REMOVAL EFFICIENCIES ARE 99.5 AND
60 PERCENTt RESPECTIVELY.
     EACH BOILER IS EQUIPPED WITH THREE SCRUBBER MODULES, EACH MODULE CAPABLE OF HANDLING 40 PERCENT OF THE BOILER FLUE GAS
CAPACITY (1.430,000 ACFM AT 291F).  EACH SCRUBBER MODULE INCORPORATES A VARIABLE-THROAT VENTURI  (DESIGN SUPERFICIAL GAS VELOCITY*
200 FT/SEC), A SPRAY ABSORPTION SECTION (DESIGN SUPERFICIAL GAS VELOCITY* 11.5 FT/SEC), AN INTERNAL RECYCLE TANK, A WASH TRAY,
AND A CHEVRON-TYPE MIST ELIMINATOR.  THE VENTURI AND SPRAY SECTIONS OPERATE ON A RECIRCULATING SLURRY LOOP CONTAINING 12 PERCENT
SOLIDS (CONSISTING PRIMARILY OF CALCIUM SALTS AND FLY ASH).  TOTAL MODULE PRESSURE DROP IS APPROXIMATELY 23.5 INCHES H20.  TOTAL
MODULE LIQUID-TO-GAS RATIO is APPROXIMATELY 33 GAL/IOOO ACF.  A WASH  TRAY is SITUATED BENEATH  THE MIST ELIMINATOR IN ORDER TO
DILUTE ANY ENTRAINMENT REACHING THE COMPONENT, THUS REDUCING THE POTENTIAL FOR PLUGGING AND SCALING.  THE TRAY OPERATES OFF A
SEPARATE RECYCLE TANK AND RECIRCULATION LOOP.  REHEAT IS SUPPLIED BY  IN-THE-FLUE-GAS-STREAM STEAM TUBE BUNDLES (MINIMUM DELTA T*
50 F>>  THE REHEATERS ARE ALSO EQUIPPED WITH SOOT BLOWERS FOR CLEANING.  THE SCRUBBER BOOSTER  FANS (INDUCED DRAFT, 43.5 INCHES
H20) ARC LOCATED DOWNSTREAM OF THE SCRUBBERS AND OPERATE ON DRY, REHEATED FLUE GAS.  THE FANS  WERE LOCATED DOWNSTREAM IN THIS
SCRUBBER DESIGN BECAUSE OF THE HIGH PARTICULATE LOADING OF TH£ INLET  FLUE GAS.  THE SCRUBBING  WASTES (UNREACTEO FLY ASH, 9 PARTS
CALCIUM SULFATE/1 PART CALCIUM SULFITE) ARE DISCHARGED TO AN INITAL HOLDING BASIN (520  ACRE-FEET) ADJACENT TO THE SCRUBBER PLANT

                                                               146
                                                                                           PEDCo  ENVIRONMENTAL
                                                                                                  CINCINNATI. OHIO 45246

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COLSTRIP (CONTINUED!

AND THEN PUPPED (50.8 DRY TPH/2 UNITS) THREE MILES TO A PERMANENT SLUDGE DISPOSAL POND (2218 ACRE-FEETt CLAY-LINED WHERE NECESS-

ARY).  CLEAR LIQUOR IS RETURNED FROM PONDS FOR ADDITIONAL SCRUBBING SERVICE.  FRESH MAKE-UP WATER TO THE SYSTEM IS LIMITED TO

APPROXIMATELY THE AMOUNT OF WATER LOST IN THE SCRUBBER PLANT VIA EVAPORATION AND SLUDGE.

PERFORMANCE HISTORY*

UNIT NO.l BECAME AVAILABLE FOR SERVICE DURING THE LATTER PA>*T OF 1975.  UNIT NO.2 WAS PLACED IN SERVICE DURING THE SUMMER OF 1976.

INFORMATION AND DATA CONCERNING PERFORMANCE OF THE SCRUBBER PLANTS HAVE NOT BEEN MADE AVAILABLE BY THE UTILITY.  CEA/ADL HAS

REPORTED SUCCESSFUL AND RELIABLE OPERATIONS FOR BOTH SCRUBBER PLANTS SINCE START-UP.
                                                                                          PEDCo  ENVIRONMENTAL
                                                                                                 CINCINNATI. OHIO

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                  TABLE  5
PERFORMANCE DESCRIPTION  FOR  OPERATIONAL  F6D SYSTEMS   06/77
 IDENTIFICATION  NO.

 UTILITY NAME

 UNIT NAME

 UNIT LOCATION

 UNIT RATING

 FUEL CHARACTERISTICS

 FGO VENDOR

 PROCESS

 NEW OR  RETROFIT

 START UP DATE

 FGD STATUS

 EFFICIENCY.
  PARTICULATES
  62

 NEVADA POWER

 REIO GARDNER NO i

 MOAPA NEVADA

  125 MW

 COAL 0.5 - 1.0 PERCENT SULFUR

 ADL/COMBUSTION EQUIP ASSOCIATE

 SODIUM CARBONATE SCRUBBING

 RETROFIT
 OPERATIONAL


 99 PERCENT
  S02
 85 PERCENT
 WATER  MAKE  UP
 OPEN LOOP 1.52 GPM/Mk,
 SLUDGE  DISPOSAL
 UNSTABILIZED SLUDGE DISPOSED IN UNLINED POND
 UNIT COST
Si»if/KW (1974 DOLLARS) * $600«OSfcOO. 000 ANNUALIZED
 OPERATIONAL
 EXPERIENCE
 REFER TO THE BACKGROUND INFORMATION SECTION IN TABLE 5 OF THIS REPORT.
 THIS SODIUM CARBONATE-BASED (TRONA) SCRUBBING SYSTEM CONSISTS OF ONE
 MODULE CONTAINING A TWIN VARlABLE-THKOAT VENTURI SCRUBBER FOLLOWED BY A
 SEPARATOR IN SERIES WITH A SINGLE-STAGE PERFORATED-PLATE ABSORBER TOWER.
 THE MODULE WAS FIRST PLACED IN SERVICE ON BOILER FLUE GAS IN APHIL 1971*.
 DURING THE REPORT PERIOD THE SCRUBBER WAS UNAVAILABLE FOR SERVICE BECAUSE
 OF REPAIRS TO DAMAGED LINER MATERIAL. THE SYSTEM IS SCHEDULED TO BE BACK
 IN OPERATION BY MID-JUNE.
                                                                                       PEDCo  ENVIRONMENTAL
                                                                                              CINCINNATI. OHIO  45246

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                  TABLE 5
PERFORMANCE: DESCRIPTION FOR OPERATIONAL FGD SYSTEMS  oe/77
 IDENTIFICATION NO.

 UTILITY NAME

 UNIT NAME

 UNIT LOCATION

 UNIT RATING

 FUEL CHARACTERISTICS

 FGO VENDOR

 PROCESS

 NEW OR RETROFIT

 START UP DATE

 FGO STATUS

 EFFICIENCY*
  PARTICULATES
  63

 NEVADA  POWER

 REID GARDNER NO 2

 MOAPA NEVADA

  125 MM

 COAL 0.5 - 1.0 PERCENT  SULFUR

 AOL/COMBUSTION EQUIP ASSOCIATE

 SODIUM  CARBONATE SCRUBBING

 RETROFIT
 OPERATIONAL
 99 PERCENT
  S02
 65 PERCENT
 WATER MAKE UP
 OPEN LOOP  1.52 GPM/MH
 SLUDGE DISPOSAL
 UNSTABILIZED SLUDGE DISPOSED IN UNLINED POND
 UNIT COST
Sl»i»/KW(197t DOLLARS)* S600.00000 ANNUALIZEO
 OPERATIONAL
  EXPERIENCE
 REFER TO THE BACKGROUND INFORMATION SECTION IN TABLE s OF THIS REPORT.
 THIS SODIUM CARBONATE-BASED (TRONA) SCRUBBING SYSTEM CONSISTS OF ONE
 MODULE CONTAINING A TWIN VARIABLE-THROAT VENTURI SCRUBBER FOLLOWED By A
 SEPARATOR IN SERIES WITH A SINGLE-STAGE PERFORATED-PLATE ABSORBER TOWER.
 THE MODULE WAS FIRST PLACED IN SERVICE ON BOILER FLUE GAS IN APKIL 197H.
 DURING THE REPORT PERIOD THE SYSTEM WAS IN SERVICE WITH THE EXCEPTION OF
 A 2-taEEK BOILEK OUTAGE FOR flAlNTAlNENCE AND REPAIRS.
                                                            1<*9
                                                                                       PEDCo  ENVIRONMENTAL
                                                                                              CINCINNATI. OHIO

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                  TABLE  5
PERFORMANCE DESCRIPTION  FOR OPERATIONAL FGD SYSTEMS  Ofc/77
 IDENTIFICATION NO.
 UTILITY  NAME
 UNIT NAME
 UNIT LOCATION
 UNIT RATING
 FUEL CHARACTERISTICS
 FGO  VENDOR
 PROCESS
 NEW  OR RETROFIT
 START UP DATE
 FGD  STATUS
 EFFICIENCY,
 PARTICULATES
NEVADA POWER
REID GARDNER NO 3
MOAPA NEVADA
 125 MW
COAL 0.5 - 1.0 PERCENT SULFUR
ADL/COMBUSTION EQUIP ASSOCIATE
SODIUM CARBONATE SCRUBBING
NEW
 7/76
OPERATIONAL

99 PERCENT
  S02
65 PERCENT
 WATER MAKE UP
 SLUDGE DISPOSAL
OPEN LOOP 1.52 GPM/HW
UNSTABILIZED SLUuGE DISPOSED IN UNLlNED POND
UNIT COST
 OPERATIONAL
 EXPERIENCE
REFER TO THE BACKGROUND INFORMATION SECTION IN TABLE 5 OF THIS REPORT.
THIS UNIT IS A NEW COAL-FIRED BOILER THAT IS EQUIPPED WITH SODIUM
CARBONATE-BASEU(TRONA»SCRUBBING SYSTEM WHICH INCORPORATES A TWIN
VARIABLE-THROAT VENTURI SCRUBBER FOLLOWED BY A SEPARATOR IN SERIES WITH
A SINGLE-STAGE PERFORATED-PLATE ABSORBER TOWER.  THE MODULE WAS FIRST
PLACED IN SERVICE ON BOILER FLUE GAS IN JULY 1976.  DURING THE PERIOD
THE SYSTEM WAS OPERATIONAL IN APRIL AND DOWN IN MAY FOR A 3-WEEK OUTAGE
FOR AN FRP LINER REPLACEMENT IN THE SEPARATOR.
                                                           150
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                                                     BACKGROUND INFORMATION
                                                                ON
                                                 HEIU OARDNER UNITS 1, 2t AND 3
     THE REID GARDNER POWER STATION IS LOCATED NEAR MOAPA. NEVADA, ABOUT 50 MILES NORTH OF LAS VEGAS.  THE STATION HAS THREE
ELECTRIC POWER GENERATING UNITS. CREID GARDNER i, 2. AND 3) EACH RATED AT 125 nw.  UNITS i AND 2 ARE RETROFITTED WITH sooiun
CARBONATE-BASED FGO SYSTEMS.  UNIT NO. s is A NEW INSTALLATION. ALSO EQUIPPED WITH A SODIUM CARBONATE-BASED FGD SYSTEM.  THE COAL
BURNED AT THE PLANT HAS AN AVERAGE GROSS HEATING VALUE Qf 12.450 BTU/LB. AND ASH AND SULFUR CONTENTS OF 8 AND 0.5 PERCENT RESPEC-

TIVELY*
     THE FGD SYSTEMS INSTALLED ON REID GARDNER UNITS i, 2, AND s WERE DESIGNED AND INSTALLED BY COMBUSTION EQUIPMENT ASSOCIATES IN
ASSOCIATION WITH A.D. LITTLE.  THE SYSTEMS FOR UNITS 1 AND 2 WERE PLACED IN SERVICE IN APRIL 197"».  THE SYSTEM FOR UNIT 3 WAS
PLACED IN OPERATION ON JULY 12, 1976.  THE SCRUBBING SYSTEM DESIGN WAS BASED ON INFORMATION AND DATA OBTAINED FROM AN 8000-ACFM
PILOT PLANT PROGRAM CONDUCTED AT THIS STATION IN 1971 AND 1972.
     THE FGD SYSTEM CONSISTS OF A SINGLE MODULE, DESIGNED TO HANDLE «*73.000 ACFM OF GAS AT 350 F.  THE MODULE IS MADE UP OF A TWIN
VARIABLE-THROAT VENTURI SCRUBBER, FOLLOWED BY A SINGLE-STAGE WASH TRAY.  BYPASSING OF THE MODULE IS POSSIBLE THROUGH A GUILLOTINE-
TYPE BY-PASS.  A COMMON FACILITY FOR TRONA (SODIUM CARBONATE ORE) STORAGE AND SAND REMOVAL SERVES ALL THE FGD MODULES AT THE REID
GARDNER PLANT.  SULFUR DIOXIDE REMOVAL EFFICIENCY IS REPORTED  TO BE 85 PERCENT.  PRIMARY PARTICULATE REMOVAL IS ACCOMPLISHED BY 75
PERCENT EFFICIENT MECHANICAL COLLECTORS INSTALLED UPSTREAM OF  THE WET SCRUBBERS.  THE TOTAL PARTICULATE REMOVAL EFFICIENCY OF THE
MECHANICAL COLLECTION AND WET SCRUBBING SYSTEM EXCEEDS THE 99  PERCENT LEVEL.
     IN THIS SODIUM CARBONATE PROCESS, HOT FLUE GAS FROM  THE BOILER PASSES FIRST THROUGH THE MECHANICAL COLLECTORS WHERE PRIMARY
PARTICULATE REMOVAL TAKES PLACE.  PRESSURE IS THEN BOOSTED BY  AN INDUCED DRAFT FAN BEFORE THE GAS STREAM SPLITS AS IT ENTERS THE
TWIN-THROAT VENTURI SCRUBBER.  THE HOT FLUE GAS IS QUENCHED BY A SHOWER OF CIRCULATED SODIUM.BASE LIQUOR.  THE GAS THEN ENTERS THE
WASH TRAY AND BUBBLES THROUGH THE RADIAL-VANE MIST ELIMINATOR, WHERE THE REMAINING LIQUID DROPLETS CARRIED OVER WITH THE GAS ARE

TRAPPED AND REMOVED.
     EFFLUENT FROM THE F6D  SYSTEM IS FROM TWO SOURCES*  THE SLIP STREAM OF SPENT LIQUOR DISCHARGED FROM THE RECIRCULATION TANK,
AND THE ALKALINE CLARIFIER  UNDERFLOW, WHICH SERVES TO NEUTRALIZE THE PH OF THE COMBINED LIQUOR BEFORE IT IS DISCHARGED TO THE
SLUDGE SETTLING PONDS.  THE SPENT LIQUOR Is PUMPED INTO ONE OF TWO SETTLING PONDS.  THE OVERFLOW FROM THIS POND Is PUMPED TO A
LARGER «>5-ACRE POND, WHERE  THE BRINE IS EVAPORATED.  THE  FGD SYSTEM OPERATES ON AN OPEN WATER LOOP WITH NO LIQUOR RECYCLED TO THE


                                                               151
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REID GARDNER UNITS 1,  2.  AND  3  (CONTINUED)

MODULES FROM THE PONDS.

     ADDITIONAL INFORMATION CONCERNING  THE  PERFORMANCE  OF  THE  SCRUBBERS  INSTALLED AT THE REID GARDNER STATION,  INCLUDING PROBLEMS,

SOLUTIONS,  AND MODIFICATIONS, ARE  PRESENTED IN  THE  FOLLOWING  TABLES.   IN ADDITION,  A GENERAL PROCESS FLOW DIAGRAM OF THE SODIUM

CARBONATE SCRUBBING SYSTEM IS PRESENTED IN  APPENDIX B
                                                               152

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                                                          REID GARDNER 1
PERIOD

MAR. 75
APR. 75
MAY  75
JUN. 75
                  BOILER
          TOTAL  OPERATION
          (HR.I    (HR.)
                HR.
              CALLED
AVAILABILITY  UPON TO
   (HR.)      OPERATE
OPERATION
  «HR. >
JUL. 75
AU6. 75
SEP. 75    720      716
OPERABILITY * 78*
UTILIZATION = 78*
OCT. 75    7«H»      303
OPERABILITY = 60*
UTILIZATION = 1<*X
NOV. 75    720      65«»
OPERABILITY = 60*
UTILIZATION = 55*
DEC. 75
                           559
                           106
                           39H
                         COMMENTS
DURING FEBRUARY THE FGD SYSTEM OPERATED WITH 95 PERCENT AVAILA-
BILITY ON TRONA SUPPLEMENTED WITH SODA ASH.  AVAILABILITY IN
JANUARY WAS ONLY ABOUT 65 PERCENT BECAUSE OF FROZEN SODIUM
CARBONATE FEED LINES.  PROBLEMS IN FEBRUARY INCLUDED A 2-DAY
LACK OF CHEMICALS.  NO SIGNIFICANT PROBLEMS OCCURRED IN MARCH.
THE UNIT RAN APRIL 1 THROUGH APKIL 12 WITH 100 PERCENT AVAILA-
BILITY.  THE BOILER WAS THEN SHUT DOWN FOR ROUTINE MAINTENANCE.
THE SYSTEM WAS PLACED BACK ON LINE MAY 12.  SECOND PERFORMANCE
TEST WAS PASSED.  PROBLEMS INCLUDED ABRASION OF RUBBER-LINED
PIPES AND ROUTINE MECHANICAL AND  INSTRUMENTAL PROBLEMS.  HIGH ASH
CONTENT. UP TO 20 PERCENT, HAD NO EFFECT ON EMISSIONS.
OPERABILITY FOR THE MONTH OF JULY WAS 85 PERCENT.

OF FOUR FORCED OUTAGES. THREE WERE CAUSED BY SCRUBBER MALFUNC-
TIONS.

LOW OPERATING TIME WAS DUE TO SCHEDULED BOILER MAINTENANCE.  ONE
OUTAGE WAS DUE TO THE MALFUNCTION OF A SODA ASH BLOWER.

THE UTILITY REPORTS SYSTEM PERFORMANCE IN TERMS OF THE OPERA-
BILITY INDEX.  UNIT NO. 1 OPERABILITY WAS LOW FOR THE MONTH OF
NOVEMBER BECAUSE OF DELAYS IN DELIVERY OF REPAIR MATERIALS.
THREE FORCED OUTAGES DURING THE MONTH WERE DUE TO REHEATER STEAM
                                                               153
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                                                    REID GARDNER 1  (CONTINUED)
PERIOD
                  BOILER
          TOTAL  OPERATION
          (HR.I    (HP.)
JAN. 76    7«t«»      6<»7

AVAILABILITY = SIX

OPERABILITY = 291

RELIABILITY = 57*

UTILIZATION = 25*

FEB. 76    696      66
-------
                                                    REID GARDNER 1 (CONTINUED)
                  BOILER
          TOTAL  OPERATION
          (HR.»    8
                                  COMMENTS




         THE NO. 1 UNIT UAS SHUT DOWN THE ENTIRE MONTH FOR A SCHEDULED

         TURBINE OVERHAUL AND BURNER LINE CONDUIT REPLACEMENT.

         THE NO. 1 UNIT REMAINED OUT OF SERVICE THROUGHOUT THE MONTH FOR

         COMPLETION OF THE TURBINE AND BOILER OVERHAUL WHICH COMMENCED THE

         PRECEDING MONTH.

         TWO FORCED SCRUBBER OUTAGES OCCURRED DURING THE MONTH ATTRIBUTED

         TO PLUGGING IN THE TRAY RECYCLE TANK AND THICKENER TANK.  TOTAL

         BOILER OUTAGE TIME FOR THE MONTH EXCEEDED 265 HOURS.
TWO FORCED SCRUBBER OUTAGES WERE REPORTED BY THE UTILITY FOR THE

MONTH.  THESE MINOR OUTAGES WERE CAUSED BY PLUGGING IN THE

VENTURI SPRAY HEADERS AND AN I.D. FAN MALFUNCTION.  TOTAL FORCED

OUTAGE TIME AMOUNTED TO 36.8«» HOURS.



SCRUBBER OUTAGE TIME WAS REQUIRED FOR INSTALLATION OF A NEW CAR-

 BONATE FEED LINE.  IN ADDITION. A MINOR SCRUBBER TRIP WAS CAUSED

BY PLUGGING IN THE SCRUBBER EFFLUENT SUCTION LINE.
                                                               Ibi
                                                                                           PEDCo  ENVIRONMENTAL.
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                                                    REID GARDNER 1 (CONTINUED)
                  BOILER
          TOTAL  OPERATION
PERIOD     HR.      HR.

NOV. 76    720     631

AVAILABILITY = 87*

RELIABILITY = 6tX

OPERABILITT = 81*

UTILIZATION = 71X

DEC. 76    7«»<»     677

AVAILABILITY = 93X

RELIABILITY s 92X

OPERABILITY = 681

UTILIZATION = 80X

JAN. 77    7«»«»     6
-------
                                                         REID GARDNER 2
PERIOD

FEB. 75

MAR. 75

APR. 75

HAY  75

JUN. 75
                  BOILER
          TOTAL  OPERATION
          (HR.)    (HR.I
                HR.
              CALLED
AVAILABILITY  UPON TO
   (HH.)      OPERATE
        OPERATION
          (HH. )
JUL. 75

AUG. 75

SEP. 75     720      6«5

OPERABILITY = 77*

UTILIZATION = 69*

OCT. 75     7i»U      531

OPERABILITY = 87*

UTILIZATION = 62*

NOV. 75     720      603

OPERABILITY = 99*

UTILIZATION = 83*




DEC. 75

JAN. 76     74i»      691

AVAILABILITY = 72*

RELIABILITY r 66*
                           596
    535
691
458
                         COMMENTS

DURING FEBRUARY THE FGD SYSTEM OPERATED WITH 90 PERCENT OPERA-

BILITY ON TRONA SUPPLEMENTED WITH SODA ASH.  PROBLEMS INCLUDED

A PLUGGED RECYCLE LINE STRAINER. SEAL WATER FILTERS. AND BOILER

CONTROLS.  UNIT HAS RESTARTED AFTER SHUTDOWN FOR 5-YEAR TURBINE

OVERHAUL.  SECOND PERFORMANCE TEST WAS PASSED.  PROBLEMS

INCLUDED ABRASION OF RUBBER-LINED PIPES AND ROUTINE MECHANICAL

AND INSTRUMENTAL PROBLEMS.  HIGH ASH CONTENT. UP TO 20*. HAD NO

EFFECT ON EMISSIONS.

THE FGD SYSTEM OPERABILITY FOR THE MONTH OF JULY WAS 85 PERCENT.



THREE FORCED SCRUBBER OUTAGES OCCURRED BECAUSE OF STRAINER

PLUGGING, BROKEN BUCKET ELEVATOR, WORN RECIRCULATION PIPING, AND

RUBBER LINER LEAKAGE.

THREE FORCED SCRUBBER OUTAGES WERE REPORTED FOR THE MONTH OF

OCTOBER BECAUSE OF PUMP REPAIR, INSTRUMENT PLUGGING. AND REPAIR

OF SYSTEM PIPING LEAKAGE.

THE UTILITY PREFERS TO REPORT SYSTEM PERFORMANCE IN TERMS OF THE

OPERABILITY INDEX BECAUSE OF EASE OF CALCULATION, REQUIRES NO

JUDGMENTt AND REFLECTS THE ACTUAL PERFORMANCE OF THE FGD SYSTEMS

ACCURATELY IF THE REASONS FOR DOWNTIME ARE KNOWN.



BOILER WAS OUT OF SERVICE A TOTAL OF 3 DAYS DURING THE MONTN.

SCRUBBER OUTAGES WERE CAUSED BY FROZEN CARBONATE LINES, PLUGGED

PRESSURE-SENSING LINES. DUCT PRESSURE TRIPS. AND OVERHAUL OF A
                                                               157
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                                                    REID GARDNER 2 (CONTINUED!
                  BOILER
          TOTAL  OPERATION
PERIOD    (HR.)    CHR.)

OPERABILITY = 66*

UTILIZATION = 62«

FEB. 76    696       675

AVAILABILITY = 8"**

RELIABILITY s 86*

OPERABILITY = 86*

UTILIZATION = 631

MAR. 76     7H«f      660

AVAILABILITY = 67*

RELIABILITY = 62*

OPERABILITY = 60*

UTILIZATION = 53»

APR. 76     720      629

AVAILABILITY = 86*

RELIABILITY = 631

OPERABILITY = 77*

UTILIZATION = 68*

HAY  76

JUN. 76    720       662

AVAILABILITY = 99*

RELIABILITY = 98*

OPERABILITY = 83*

UTILIZATION = 79*
AVAILABILITY
   (HR.)
    582
  HR.
CALLED
UPON TO
OPERATE
  675
OPERATION
  (HR. I
   578
    «»95
  633
   395
    622
                           H86
                579
                           568
                                                             COMMENTS
                                    TRAY RECYCLE PUMP.
THE UTILITY REPORTED FOUR SCRUBBER INACTIVE PERIODS DURING THE

MONTH, THREE OF WHICH WERE SCRUBBER-RELATED OUTAGES.  THE FORCED

SCRUBBER OUTAGES OCCURRED BECAUSE OF PLUGGING IN A VENTURI PUMP.

DEPLETION OF CHEMICAL, CHEMICAL LINE PLUGGING, AND SEAL WATER

PROBLEMS.

TWO FORCED SCRUBBER OUTAGES WERE REPORTED FOR THE MONTH BECAUSE

OF AN ELECTRICAL FAILURE AND PLUGGING IN THE TRAY SYSTEM

RESULTING IN A SUBSEQUENT OVERHAUL OF THE TRAY RECYCLE PUMPS.
                      FOUR FORCED SCRUBBER OUTAGES HERE REPORTED BY THE  UTILITY  FOR

                      APRIL.  PROBLEMS ENCOUNTERED WERE*  PLUGGED  SENSING  LINES,  A

                      REHEATER LEAK, VENTURI SPOOL RECYCLE REPLACEMENT.  AND  TANK

                      PATCHING.
                      PROBLEMS ENCOUNTERED DURING THE MONTH  INCLUDED  PLUGGED  VENTURI

                      LINES AND A PLUGGED SENSING LINE.  TOTAL SCRUBBER  OPERATION  TIME

                      TO DATE IS 9,«66 HOURS.
                                                               158
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                                                    REID GARDNER Z (CONTINUED)
                  BOILER
          TOTAL  OPERATION
PERIOD    (HR.)    (HR.)

JUL. 76    744      518

AVAILABILITY = 91*

RELIABILITY = 96*

OPERABILITY £ SIX

UTILIZATION s 57*

AUG. 76    744       709

AVAILABILITY = 95*

RELIABILITY s 94X

OPERABILITY r 75X

UTILIZATION * 71*

SEP. 76    720       681

AVAILABILITY = 94*

RELIABILITY = 94*

OPERABILITY s 96X

UTILIZATION s 91X

OCT. 76    744       694

AVAILABILITY = 93*

RELIABILITY = 95X

OPERABILITY s 95X

UTILIZATION = 88X
                HR.
              CALLED
AVAILABILITY  UPON TO
   (HR.)      OPERATE
    676
43
OPERATION
  (HR.)

   421
    710
564
           530
    677
697
                           653
    706
692
   656
                         COMMENTS

TWO FORCED SCRUBBER OUTAGES WERE REPORTED DURING THE MONTH.  A

PROBLEM WITH A HIGH SOLIUS CONCENTRATION IN THE VENTURI SCRUBBING

CYCLE AND THE REPLACEMENT OF A RUBBER-LINED PIPE IN THE VENTURI

SCRUBBER RESULTED IN AN OUTAGE TIME OF APPROXIMATELY 19. HOURS.



FORCED SCRUBBER OUTAGE TIME TOTALLED 34.5 HOURS.  TWO TRIpS

OCCURRED DURING THE MONTH BECAUSE OF LEAKAGE IN THE VENTURI

RECYCLE LINE AND PLUGGING IN THE THICKENER TANK.  THE REMAINING

SCRUBBER OUTAGE TIME DURING THE MONTH RESULTED FROM DEPLETION

OF CHEMICAL ABSORBENT (TRONA) AND BOILER TRIPS.

TWO FORCED SCRUBBER OUTAGES, TOTALING 43.5 HOURS OF OUTAGE TIME,

WERE REPORTED BY THE UTILITY DURING THE MONTH.  MINOR TRIPS WERE

CAUSED BY PLUGGING IN THE I.D. FAN REFERENCE LINES AND A FALSE

HIGH TEMPERATURE READING IN THE VENTURI CAUSED BY WATER IN THE

INSTRUMENT.

TOTAL FORCED OUTAGE TIME FOR THE MONTH AMOUNTED TO APPROXIMATELY

36 HOURS.  SCRUBBER TRIPS WERE CAUSED BY VENTURI GAS DAMPER

PROBLEHS. PLUGGING IN THE SCRUBBER EFFLUENT LINE, AND REPLACEMENT

OF THE CARBONATE FEED LINE.  SCRUBBER OUTAGE TIME DUE TO BOILER

TRIPS AMOUNTED TO APPROXIMATELY 65 HOURS.
                                                               159
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                                                    REID GARDNER 2 (CONTINUED)
                  BOILER
          TOTAL  OPERATION
           HR.      HR.
NOV. 76     720      621
AVAILABILITY = 52X
RELIABILITY = 51*
OPERABILITY = 5B«
UTILIZATION s 50X
DEC. 76     7<»i»      275
ALL INDEX VALUES = OX
JAN. 77    7"»«»        0
ALL INDEX VALUES = OX
FEB. 77    672       516
AVAILABILITY = 93X
RELIABILITY s 88X
OPERABILITY = 75X
UTILIZATION = 56X
MAR. 77    7«m       659
AVAILABILITY = 92X
RELIABILITY = 97X
OPERABILITY = 66X
UTILIZATION = 76X
APR. 77
MAY 77
                HR.
              CALLED
AVAILABILITY  UPON TO   OPLRATION
    HR.       OPERATE      HR.
   371*
709
                           363
   623
H31
387
   688
585
                           567
         DURING A BOILER OUTAGE TO REPAIR A CONDENSER TUBE LEftK AND
         BOTTOM ASH NoZZLEt THE SCRUBBER'S GUILLOTINE DAMPERS WERE BADLY
         DAMAGED, AND THE SCRUBBER REMAINED OUT OF SERVICE DURING THE
         MONTH OF DECEMBER.
THE BOILER WAS OFF-LINE DURING
JANUARY FOR MAINTENANCE.
TWO. MINOR SCRUBBER OUTAGES RESULTED FROM A
VENTURI PIPING LEAK AND WASH TRAY RECYCLE
TANK CLEANING.  AT THE ENU OF THE MONTH,
THERE WERE SOME ELECTRICAL PROBLEMS.

MINOR SCRUBBER OUTAGES WERE A RESULT OF
ELECTRICAL PROBLEMS, A PLUGGED SPRAY TRAY,
DUCT PRESSURE SWINGING, AND AN I.D. FAN SWING.
                                    THE SYSTEM WAS IN SERVICE DURING  THE  REPORT  PERIOD  WITH THE EX-
                                    CEPTION OF A 2-WEEK BOILER MAINTAINENCE  PERIOD.  OPERATING DATA
                                    AND INFORMATION WAS NOT PROVIDED  BY NPCO FOR THE APRIL - MAY
                                    PERIOD, BUT WILL BE AVAILABLE FOR THE NEXT REPORT.
                                                               160
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                                                          REID  GARDNER  3
                  BOILER
          TOTAL  OPERATION
PERIOD    
-------
                                                    REID GARDNER 3 (CONTINUED)
                  BOILER
          TOTAL  OPERATION
PERIOD     HR.      HR.

NOV. 76    720      26"»

AVAILABILITY = 28*

RELIABILITY = 29*

OPERABILITY = 60*

UTILIZATION c 29*

DEC. 76    7HH      7H4

AVAILABILITY = 99*

RELIABILITY = 991

OPERABLIITY = 97»

UTILIZATION = 97X

JAN. 77    7H<»      690

AVAILABILITY = 96X

RELIABILITY = 98*

OPERABILITY = 96%

UTILIZATION = 91*

FEB. 77    672      575

AVAILABILITY = 81*

RELIABILITY = 72*

OPERABILITY = 74*

UTILIZATION = 63*
                HR.
              CALLED
AVAILABILITY  UPON TO
    HR.       OPERATE.
    205
727
OPERATION
   HR.

   212
    737
728
   721
    731
689
                           676
                59H
                           422
                         COMMENTS

THE SCRUBBER SYSTEM HAS NOT IN OPERATION THE FIRST HALF OF

NOVEMBER DUE TO REPAIRS OF LEAKS IN THE VENTURI SCRUBBER BOX.

THE SYSTEM WAS RESTARTED NOV. 19. AND EXPERIENCED ONE

FORCED OUTAGE, BECAUSE OF A SCREW CONVEYOR MALFUNCTION, PRE-

VENTING CHEMICAL MIXING.

DURING THE MONTH, ONE MINOR SCRUBBER OUTAGE OCCURRED BECAUSE OF

REPAIRS TO THE I.D. FAN EXPANSION JOINT.
            TWO MINOR FORCED OUTAGES WERE THE RESULTS OF A

            PLUGGED TRAY AND A REHEATER STEAM LEAK.
                    A TOTAL OF 117 HRS. OF DOWNTIME WAS THE RESULT

                    OF THREE FORCED SCRUBBER OUTAGES CAUSED BY

                    PROBLEMS WITH THE UPPER TRAY. A FOURTH OUTAGE

                    RESULTED FROM DOWNTIME FOR CLEANING OUT THE

                    SODIUM CARBONATE LINE.
                                                               162
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                                          REID  GARDNER  3  (CONTINUED)
        BOILER
TOTAL  OPERATION
           HR .

MAR. 77    7«H»
AVAILABILITY =
RELIABILITY = 52*
OPERABILITY = 51*
UTILIZATION = <*«**

APR. 77
AVAILABILITY =
RELIABILITY =
OPERABILITY r
UTILIZATION =
MAY 77

AVAILABILITY =
RELIABILITY s
OPERABILITY =
UTILIZATION s
          HR .

          639
                HR.

              CALLED

AVAILABILITY  UPON TO
    HR.       OPERATE
    321
627
OPERATION
   HR.
   32
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                  TABLE  5
PERFORMANCE  DESCRIPTION  FOR  OPERATIONAL  f&0  SYSTEMS   06/77
 IDENTIFICATION NO.
 UTILITT  NAME
 UNIT NAME
 UNIT LOCATION
 UNIT RATING
 FUEL CHARACTERISTICS
 FGO VENDOR
 PROCESS
 NEW OR RETROFIT
 START UP DATE
 FGD STATUS
 EFFICIENCYt
  PARTICULATES
  72
 NORTHERN INDIANA PUB SERVICE
 O.H.  MITCHELL NO.11
 GARY  INDIANA
  115  MW
 COAL  3.2-3.5 PERCENT SULFUR
 DAVY  POWERGAS/ALLIEO CHEMICAL
 WELLMAN LORD/ALLIED CHEMICAL
 RETROFIT
  6/77
 OPERATIONAL

 99.5 PERCENT
  S02
 WATER MAKE UP
 90 PERCENT GUARANTEE
 CLOSED LOOP
 SLUDGE DISPOSAL
 UNIT COST
S129/KW (NETI CAPITAL * 8.1 MILLS/KWH OPERATING <1976)
 OPERATIONAL
  EXPERIENCE
 REFER TO THE BACKGROUND INFORMATION SECTION IN TABLE 5 OF THIS REPORT.
 THIS FGO SYSTEM IS AN INTEGRATION OF THE WELLHAN-LORD S02 RECOVERY PROCES
 OFFERED BY DAVY POWERGAS AND THE SOg TO SULFUR REDUCTION PROCESS DE-
 VELOPED BY ALLIED CHEMICAL. DAVY POWERGAS IS THE DESIGN AND CONSTRUCTION
 FIRM AND ALLIED CHEMICAL IS SYSTEM OPERATOR AND PRODUCT MARKETER.
 DURING THE REPORT PERIOD THE DEMONSTRATIUN SCRUBBER PLANT WAS STARTED UP
 AND OPERATED AT APPROXIMATELY 60 PERCENT FLUE GAS CAPACITY BECAUSE OF
 AIR PREHEATER PROBLEMS  IN THfc. BOILER.
                                                            164
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                                                      BACKGROUND INFORMATION
                                                                ON
                                                       D.H. MITCHELL NO. 11
     IN JUNE OF 1972 THE NORTHERN INDIANA PUBLIC SERVICE CO. (NIPSCO) AND THE U.S. ENVIRONMENTAL PROTECTION AGENCY ENTERED INTO
A COST-SHARED CONTRACT FOR THE CONSTRUCTION AND OPERATION OF A WtLLMAN-LORD/ALLIED CHEMICAL FLUE GAS DESuLFURIZATION DEMONSTRATION
PLANT.  THE SYSTEM WAS INSTALLED ON GENERATING UNIT NO. 11 AT NIPSCO'S D.H. MITCHELL POWER STATION IN GARYt INDlANAi ON THE
SOUTHERN TIP OF LAKE MICHIGAN.  UNIT NO. 11 IS RATED AT 115 MW AND FIRES MIDWEST COAL WITH A HEAT VALUE OF 11,000 BTU/L8. AND
SULFUR AND ASH CONTENTS OF 3.5 AND 10.Ot RESPECTIVELY.
     THIS UNIT WILL BE THE FIRST RE6ENERABLE FGD SYSTEM TO CONTROL THE TOTAL FLUE GAS EMISSION FROM A FULL SCALE COAL-FIRED
GENERATING UNIT. IT WILL ALSO BE THE FIRST SYSTEM TO RECOVER ELEMENTAL SULFUR OF A MARKETABLE QUALITY FROM THE FLUE GAS OF AN
ELECTRIC UTILITY.
     THE FGD SYSTEM CONSISTS OF THREE MAJOR PROCESS UNITS* A WELLMAN-LORU S02 RECOVERY UNIT, A DAVY POWERGAS PURGE TREATMENT
UNIT, AND AN ALLIED CHEMICAL S02 REDUCTION UNIT.
     THE S02 RECOVERY SYSTEM INCLUDES A FLUE 6AS BOOSTER BLOWER, A PRESCRUBBER (ORIFICE CONTACTOR), A THREE-STAGE TRAY TOWER
ABSORBER, AND AN EVAPORATOR/CRYSTALLI2ER. THE PRESCRUBBER  IS A VAKIABLE-THROAT VENTURI USED TO SATURATE THE FLUE GAS AND REMOVE
ANY FLYASH NOT COLLECTED IN THE ESP UNIT.  THE SCRUBBING SOLUTION IS PURGED CONTINUOUSLY TO A SLUDGE POND,  THE ABSORBER IS A
THREE-STAGE MULTIVENTURI FLEXITRAY  (MVFT».ABSORPTION TOWER FOLLOWED BY A HIST ELIMINATOR AND A STACK GAS REHEATER. THE SPENT
SCRUBBING (SODIUM SULFITE-BISULFITE) SOLUTION IS REGENERATED IN AN EVAPORATOR/CRYSTALLIZER, WHERE IT IS
HEATED UNTIL THE BISULFITE DECOMPOSES, EMITTING S02 GAS AND PRECIPITATING SODIUM SULFITE CRYSTALS.  THESE ARE REMOVED AND REOIS-
SOLVED IN THE CONDENSATE FROM THE EVAPORATOR FOR RECYCLE TO THE ABSORBER.
     A SHALL SIOESTREAM IS REMOVED FROM THE SCRUBBING LI8UOR LEAVING THE ABSORBER AND SENT TO THE PURGE TREATMENT UNIT TO REMOVE
SODIUM SULFATE. THIS SYSTEM CONSISTS OF FOUR CHILLED-WALL CRYSTALLIZERS WHERE SODIUM SULFATE CRYSTALS FORM, FOLLOWED BY A CENTRI-

FUGE AND CRYSTAL DRYER.
     THE SULFUR DIOXIDE FROM THE EVAPORATOR/CRYSTALLIZER IS COMPRESSED AND SENT TO THE ALLIED CHEMICAL S02 REDUCTION PLANT, WHERE
IT IS REACTED WITH NATURAL GAS.  THE RESULTING ELEMENTAL SULFUR IS CONDENSED AND STORED IN MOLTEN FORM, WHILE THE OFF-GASES ARE
BURNED IN A TAIL GAS INCINERATOR AND RETURNED TO THE ABSORBER INLET.  THE ALLIED PLANT IS DESIGNED TO GENERATE 25 TON/DAY OF

SULFUR.


                                                               165

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D.H. MITCHELL NO.  11  «CONTINUED>

     THE PRIMARY ENGINEERING  AND  CONSTRUCTION  FIRM  IS  DAVY  POUERGAS.   ALLIED  CHEMICAL  WILL  OPERATE  THE  UNIT  AND  MARKET  THE

ELEMENTAL SULFUR AND  SODIUM SALT  BY-PRODUCTS ON  A CONTINUED BASIS.  PERFORMANCE  TESTING IS BEING  CONDUCTED  JOINTLY  BY  THESE  TWO

FIRMS, WITH TRW, INC.  MONITORING  UNDER  CONTRACT  TO  THE EPA.

     AFTER A DELAY OF  SEVERAL MONTHS  DUE  TO BOILER  UNAVAILABILITY,  THE D.H. MITCHELL UNIT NO.  11 FGD  SYSTEM  BEGAN  OPERATION

ON JUNE 13« 1977,  WITH O^NLY THE ABSORBER  IN OPERATION. ON JUNE  15,  THE FIRST  INTEGRATED OPERATION OF  THE SYSTEM  OCCURRLO.   A

16-DAY ACCEPTANCE  TEST IS EXPECTED  TO GET UNDERWAY  IN  EARLY JULY, FOLLOWED BY A 1-YEAR PERIOD  OF MONITORING  LONG-TERM EFFICIENCY

AND AVAILABILITY.   THE SCRUBBER SYSTEM  HAS BEEN  DESIGNED TO REMOVE  A  MINIMUM  OF 90  PERCENT  OF  THE S02 IN THE FLUE  GAS OR  MAINTAIN

A MAXIMUM OF 200 PP«  so2 IN THE FLUE  GASf WHICHEVER is THE  LESSER,  soz REGULATIONS REQUIRE THE  MITCHELL STATION TO COMPLY  WITH

THE EMISSION LIMITATION OF 1.2 POUNDS S02 PER  MILLION  BTU.

     REFER TO APPENDIX B FOR  A PROCESS  FLOW DIAGRAM.
                                                               166

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                  TABLE: s
PERFORMANCE DESCRIPTION FOR OPERATIONAL F6D SYSTEMS  06/77
 IDENTIFICATION NO.
 UTILITY NAME
 UNIT NAME
 UNIT LOCATION
 UNIT RATING
 FUEL CHARACTERISTICS
 F6D VENDOR
 PROCESS
 NEW OR RETROFIT
 START UP DATE
 F6D STATUS
 EFFICIENCYt
  PARTICULATES
  73
 NORTHfRN  STATES  POWER  CO.
 SHERBURNE COUNlY STATION NU.l
 BECKER- MINNESOTA
  710  MH
 COAL  0.6  PERCENT SULFUR
 COMBUSTION ENGINEERING
 LIMESTONE SCRUBBING
 NEW
  3/76
 OPERATIONAL

 99 PERCENT GUARANTEE
  S02
 50 PERCENT GUARANTEE
 HATER MAKE UP
 OPEN LOOP 1.13 GPM/MU
 SLUDGE DISPOSAL
 UNSTABILI2EO SLUDGE DISPOSED IN LINED POND
 UNIT COST
S60 MILLION CAPITAL FOR UNITS 1 AND 2
 OPERATIONAL
  EXPERIENCE
 REFER TO THE BACKGROUND INFORMATION SECTION IN TABLE s OF THIS REPORT.
 FULL COMMERCIAL OPERATION OF THE SYSTEM BEGAN ON MAY It 1976. THE SCRUB-
 BING SYSTEM FOR THIS UNIT CONSISTS OF 12 MODULES. EACH SCRUBBING MODULE
 INCORPORATES A VENTURI-ROD SECTION AND A MARBLE BED ABSORBER FOR PAR-
 TICULATE AND SULFUR DIOXIDE REMOVAL. AVAILABILITY INDEX VALUES FOR
 THE MONTHS OF APRIL AND MAY WERE 95 AND 92 PtRCENT. RESPECTIVELY. THE
 UNIT WAS TAKEN OUT OF SERVICE IN MID-MAY FOR A SCHEDULED TUKBINE/BOlLEK
 OVERHAUL. RESUMPTION OF OPERATIONS is SCHEDULED FOH MID-JUNE.
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                                                     BACKGROUND INFORMATION
                                                               ON
                                               SHERBURNE COUNTY GENERATING PLANT
     THE SHERBURNE COUNTY GENERATING PLANT OF THE NORTHERN STATES POWER COMPANY IS LOCATED ON THE MISSISSIPPI RIVER IN SHERBURNE.
COUNTY NEAR BECKERf MINNESOTA.  THIS NEW POWER GENERATING PLANT CURRENTLY HAS TWO COAL-FIRED UNITS IN SERVICE AND TWO IN THE EARLY
PLANNING STAGES.  UNIT NO. 1 IS RATED AT 710 «« AND FIRES MONTANA COLSTRIP COAL WITH A HEATING VALUE OF $300 BTU/LB, AND SULFUR,
ASH. AND MOISTURE CONTENTS OF 0.8. 9.0 AND 85.0 PERCENT. RESPECTIVELY.  IN ORDER TO MEET MINNESOTA POLLUTION CONTROL AGENCY PAR-
TICULATE AND S02 EMISSION STANDARDS OF 0.96 LBS. S02 AND 0.087 LBS. PARTICULATE PER MILLION BTU HEAT INPUT TO THE BOILER, THE UNIT
WAS FITTED WITH A LIMESTONE-BASED WET SCRUBBING SYSTEM FOR SIMULTANEOUS PARTICULATE AND S02 REMOVAL.
     THE NORTHERN STATES POWER CO., SHERBURNE NO. 1 SCRUBBER DESIGN IS BASED UPON THE RESULTS OF A PILOT PLANT TEST PROGRAM CON-
DUCTED AT COMBUSTION ENGINEERING'S (CE) KREISINGER DEVELOPMENT LABORATORY AND A PROTOTYPE SCRUBBER PROGRAM CONDUCTED JOINTLY BY
COMBUSTION ENGINEERING AND NORTHERN STATES POWER AT THE UTILITY'S BLACK DOG STATION.  THE SCRUBBING SYSTEM IS COMPRISED OF A FIRST
STAGE FIXED-ROD VENTURI SCRUBBER FOR PARTICULATE REMOVAL AND A MARBLE BED ABSORBER TO COMPLETE PARTICULATE REMOVAL AND ACHIEVE THE
NECESSARY SULFUR DIOXIDE REMOVAL. THE SCRUBBING SYSTEM HAS BEEN GUARANTEED TO REMOVE 99 PERCENT OF THE PARTICULATE MATTER ENTERING
THE SCRUBBING SYSTEM, OR MAINTAIN AN EMISSION O.OH GR/DSCF, WHICHEVER OUTLET VALUE IS GREATER.  THE SULFUR DIOXIDE DESIGN REMOVAL
EFFICIENCY IS BASED UPON THE REMOVAL OF 50 PERCENT OF THE SU(_FUR IN THE FUEL (MAXIMUM FUEL SULFUR CONTENT OF 1.2 PERCENT) OR
MAINTAIN AN EMISSION OF 200 PPM, WHICHEVER OUTLET VALUE IS GREATER.
     THE GENERAL SCENARIO OF THE SHERBURNE NO. 1 SCRUBBING SYSTEM CONSISTS OF 12 SCRUBBING MODULES, 11 OF WHICH ARE REQUIRED FOR
FULL LOAD CAPACITY.  EACH MODULE HAS A RATED FLUE GAS CAPACITY OF 200.000 TO 220.000 ACFW AT 135 F.  AN AGITATED REACTION TANK IS
LOCATED AT THE BOTTOM OF EACH SCRUBBER MODULE.  THE PURpOSE OF THE REACTION TANK IS TO ALLOW COMPLETION OF SULFUR DIOXIDE FORMA-
TION TO SULFiTE, PROVIDE FORCED OXIDATION OF SULFiTE TO SULFATE. AND FACILITATE PRECIPITATION OF CALCIUM SULFATE SOLIDS.  IN
FORCED OXIDATION, AIR IS BUBBLED INTO THE REACTION TANK, OXIDIZING SULFITE TO SULFATE.  THE SULFATE FORMED IS PRECIPITATED IN THE
REACTION TANK BY ADDITION OF GYPSUM SEED CRYSTALS.  A BLEED LINE PROVIDES THE NECESSARY SOLIDS REMOVAL TO A I&O-FOOT DIAMETER
CLARIFIER.  HERE THE WASTE SOLIDS (FLy ASH, CALCIUM CARBONATE, AND CALCIUM SULFATE) SETTLE OUT AND THE CLARIFIED WATER IS RETURNED
TO THE PROCESS.
     THE CLEANED FLUE GAS THEN PASSES THROUGH A DOUBLE ROW, TWO-PASS CHEVRON MIST ELIMINATOR.  REHEAT OF HO F IS ADDED TO THE
GAS STREAM TO PROVIDE PROTECTION TO THE DOWNSTREAM DUCTWORK. I.D. FAN, AND PLUME CONTROL BEFORE FINAL DISCHARGE TO THE ATMOSPHERE.
THE CLARIFIER UNDERFLOW IS PUMPED TO A SETTLING POND WHICH IS 45-FEET DEEP AND 62 ACRES IN AREA, WITH AN 16-INCH CLAY LINING.
                                                               168
                                                                                /V~X\
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SHERBURNE COUNTY (CONTINUED)

THE WATER IS RFCYCLED FROM THE POND BACK TO THE PROCESS.  A GENERAL FLOW DIAGRAM OF THE SHERBURNE SCRUBBER ARRANGEMENT IS PROVIDED

IN APPENDIX B

     INITIAL OPERATION OF THE SYSTEM COMMENCED MARCH 16, 1976.  FULL COMMERCIAL OPERATION COMMENCED MAY 1, 197fe.  PROBLEMS ENCOUN-

TERED DURING INITIAL STARTUP OPERATIONS HAVE INCLUDED THE USUAL MECHANICAL PROBLEMS ASSOCIATED WITH A NEW SYSTEM AND SOME PLUGGING

IN THE SCRUBBER INTERVALS.  SPECIFICALLY* PROBLEMS HAVE BEEN ENCOUNTERED IN THE SPRAY SYSTEM, REOUIRING THE DESIGN OF THE NOZZLES

TO BE CHANGED FROM PLASTIC AND RUBBER COMpUNENTS TO CERAMIC SPINNER-VANE COMPONENTS.  ALSO, SOME PLUGGING PROBLEMS HAVE BEEN

ENCOUNTERED IN THE SPRAY HEADERS, PRIMARY CONTACTOR, AND MARBLE BED. THIS HAS STEMMED LARGELY FROM THE MALFUNCTION OF THE STRAINER

SYSTEM BECAUSE OF POOR NOZZLE CONFIGURATIONS.  NSP IS CURRENTLY MAKING MODIFICATIONS IN THIS AREA.
                                                               169

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                                                        SHERBURNE NO.  i

              BOILER OPERATION TIME AND MODULE OPERABILITY
        BOILER
PERIOD   HR.    101  102  103  10«»  105  106  107  108  109  110  111   112

MAR. 76

APR. 76
HAT  76    657     62   83   81   59   72   90   57   b9   60

TOTAL SYSTEM AVAILABILITY = 86X

MEGAWATT-HOURS GENERATED = 318,050

JUN. 76    686     69   78   73   62   61   63   78   73

TOTAL SYSTEM AVAILABILITY = 8HX

MEGAWATT-HOURS GENERATED = 372,450

JUL. 76    512     60   62   71   81   60

TOTAL SYSTEM AVAILABILITY = 8"»X

MEGAWATT-HOURS GENERATED = 269,700

           705     «»6   93   51   8<+   63   76   71   84   61

TOTAL SYSTEM AVAILABILITY = 9«X

MEGAWATT-HOURS GENERATED = 421,110
                    75   72
               68   70
                                                               170
                         83
68   81   75   79   63   91
                    76   87
                        COMMENTS

      A PRELIMINARY SYSTEM CHECKOUT BY PASSING WATER AND

      AIR THROUGH THE SYSTEM WAS SUCCESSFULLY COMPLETED.

      THE SYSTEM WAS INITIALLY PLACED IN SERVICE MARCH

      16, 1976.  FIRST COMMERCIAL OPERATION COMMENCED

67    MAY 1, 1976.  THIS IS AN INTERMEDIATE LOAD UNIT.

      OPERATING AT OR NEAR FULL CAPACITY DURING THE DAY

      AND 35 PERCENT CAPACITY AT NIGHT.  MODIFICATIONS

75    ARE PROCEEDING ON THE SPRAY SYSTEM, SPRAY NOZZLES,

      AND STRAINER SYSTEM.




69    DEVELOPMENTAL WORK IS CONTINUING ON THIS SCRUBBING

      SYSTEM.  SINCE JULY i, THE NO. i UNIT HAS BEEN

      GENERATING 95 TO 98 PERCENT THE NUMBER OF MW-HOURS

91    THAT HAVE BEEN REQUIRED.  THE NO. 1 UNIT IS AN

      INTERMEDIATE LOAD UNIT WHICH OPERATES AT FULL

      CAPACITY 15-16 HOURS/DAY AND ONE-THIRD CAPACITY

      THE REMAINDER.  PLUGGING IN THE SLURRY NOZZLES IS

      STILL A PROBLEM.  A QUARTER-INCH PARTICLE IN

      THE FEED SOLUTION WILL PLUG UP THE FEED NOZZLES.

      NSP is NOW PLANNING TO MODIFY THE DUPLEX STRAINER

      SYSTEM TO ALLEVIATE THIS PROBLEM.  IN ADDITION,

      THE DEPOSITION OF SOFT SOLIDS IS STILL CONTINUING

      IN THE DEMISTERS AND REHEATERS.  HARD SCALE

      GYPSUM FORMATION ON THE VESSEL WALLS HAS LEVELED

      OFF.  A CREW OF 70 PEOPLE IS REQUIRED TO MAINTAIN
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                                                              NO. 1  (CONTINUED)
        BOILER
PERIOD   HR.
              BOILER OPERATION TIME AND MODULE OPERAfalLITY
101  102  103  10<»  105  106  107  108  109  110  111  112
SEP. 76    566     87   90   93   76   76   79   85   79   85   80   92   96

TOTAL SYSTEM AVAILABILITY = 95 PERCENT

MEGAWATT-HOURS GENERATED = 3H9.«»70
OCT. 76    606     97   8*»   96   96   95   30   74   76   91   81  100

TOTAL SYSTEM AVAILABILITY s 93 PERCENT

MEGAWATT.HOURS GENERATED = 385,610
                                                          87
                  COMMENTS

SCRUBBER OPERATIONS.  THE PREVENTIVE MAINTENANCE

AND CLEANING PROCEDURES NOW EMPLOYED FOR THE

SCRUBBING SYSTEM CALLS FOR 3 TO H MODULES TO BE

TAKEN OUT OF SERVICE EACH NIGHT.  THEREFORE.

EACH MODULE IS CLEANED OUT ONCE EVERY THREE DAYS.

THE TOTAL SYSTEM AVAILABILITY INDEX IS DEFINED AS

THE AMOUNT OF TIME 11 MODULES ARE AVAILABLE TO THE

UNIT. THUS ALLOWING FULL LOAD CAPACITY CAPABILITY.

TOTAL SYSTEM OPERABILITY HAS TO BE 100 PERCENT

SINCE THE SCRUBBERS CANNOT BE BYPASSED TO OPERATE

THE BOILER. NSP IS NOW IN THE PROCESS OF MODIFYING

THE SYSTEM'S STRAINER DESIGN.  THE DUPLEX UNITS

ARE GOING TO BE RETIRED AND REPLACED WITH IN-THE-

TANK SCREENS AND SOD I BLOWERS. BOTH LOCATED AT

THE SUCTION SIDE OF THE RECYCLE PUMP.  CARBON

STEEL FIN TUBE REHEAT BUNDLES ARE ALSO AN AREA OF

CONCERN.  MULTIPLE FAILURES IN FOUR UNITS HAVE

BEEN EXPERIENCED.
                                                               171
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                                                    SHERBURNE NO.l  (CONTINUEDI
              BOILER OPERATION TIME AND MODULE AVAILABILITY
        BOILER
PERIOD     HR.    101  102  103  lot  105  106  107  108  109  110   111  112
                                            80   93   89   69   78   73
                                            97
                                                 91    95
NOV. 76    720      83    80    87    79   92
TOTAL SYSTEM AVAILABILITY =  93 PERCENT
MEGAWATT-HOURS  GENERATED = 470,820
DEC. 76    722     88   84   87    80    71
TOTAL SYSTEM AVAILABILITY = 95 PERCENT
MEGAWATT.HOURS GENERATED = 480,920
JAN. 77    607     9«»   75   99   76   96   77   70   92   81
TOTAL SYSTEM AVAILABILITY = 901
MEGAWATT-HOURS GENERATED = 386*060
FEB. 77    609     89   99   6*   96   64   99   81   62
TOTAL SYSTEM AVAILABILITY = 9lK
MEGAWATT-HOURS GENERATED = 395*210
MAR. 77    743     47   92   95   93   93   95   88   93
TOTAL SYSTEM AVAILABILITY = 95*
MEGAWATT-HOURS GENERATED = 510.650
APR. 77    718     84   65   92   95   96   62   73
TOTAL SYSTEM AVAILABILITY = 95 PERCENT
MEGAWATT-HOURS GENERATED = 460.100
MAY  77    312     96   48   92   87   95   96   81   98
88   73
                                                                          93
75
                                                                     75    95
                                                           98    93    98    61
                                                           95   83   78    72
                                                      91   58   93   90   88
                                                           96   78   35   87
                  COMMENTS
THE MODIFICATION OF THE DUPLEX STRAINER SYSTEM
IS ONGOING. CURRENTLY APPROXIMATELY ONE-THIRD
COMPLETED ON THE NO. 1 UNIT.  THE UTILITY IS
NOW CONDUCTING A FULL-LOAD EVALUATION STUDY*
ANALYZING SYSTEM OPERATION ON 10 MODULES VS.
THE DESIGNED 11 MODULES.  THE UNIT IS CURRENTLY
HAVING DIFFICULTY COMPLYING WITH THE 20 PERCENT
OPACITY REGUALTION, DUE TO THE EXTREMELY FINE
FLY ASH BEING EMITTED (70 PERCENT LESS THAN
ONE MICRON.)
LOW OPERABILITIES ARE DUE PRIMARILY TO THE COMPLE-
TION OF STRAINER MODIFICATIONS.  THESE MODIFICA-
TIONS WERE EFFECTED ONE MODULE AT A TIME.
MODULE 101 WAS THE LAST TO UNDERGO MODIFICATION
AND WORK WAS COMPLETED IN THE THIRD WEEK OF MARCH.
AT THE PRESENT TIME. ALL MODULES ARE FITTED WITH
IN-TANK STRAINERS.  THE 10 MODULE VS. 11 MODULE
EVALUATION WILL BE RESUMED IN THE NEAR FUTURE.

DURING THE REPORT PERIOD, THE UNIT WAS IN SERVICE
ONLY 13 DAYS DURING THE MONTH OF MAY BECAUSE OF A
SCHEDULED TURBINE OVERHAUL EXTENDING FROM MAY 14
TO MID-JUNLtJUNE 18 PROJECTED).
                                                               172
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                  TABLE 5
PERFORMANCE DESCRIPTION FOR OPERATIONAL FGO SYSTEMS  06/77
 IDENTIFICATION NO.
 UTILITY NAME
 UNIT NAME
 UNIT LOCATION
 UNIT RATING
 FUEL CHARACTERISTICS
 FGD VENDOR
 PROCESS
 NEW OR RETROFIT
 START UP DATE
 FGD STATUS
 EFFICIENCY,
  PARTICULATES
  7«f
 NOR  HERN  STATES POWER CO.
 SHERBUKNE COUNTY STATION NO.2
 BECKER  MINNESOTA
  680 MW
 COAL 0.8  PERCENT SULFUR
 COMBUSTION ENGINEERING
 LIMESTONE SCRUBBING
 NEW
  i»/77
 OPERATIONAL

 99 PERCENT GUARANTEE
  S02
 50 PERCENT GUARANTEE
 WATER MAKE UP
 OPEN LOOP 1.13 GPM/MW
 SLUDGE  DISPOSAL
 UNSTABILIZED SLUDGE DISPOSED IN LINED POND
 UNIT  COST
 OPERATIONAL
  EXPERIENCE
$60 MILLION CAPITAL FOR UNITS 1 AND 2
 REFER TO THE BACKGROUND INFORMATION SECTION IN TABLE 5 OF  THIS  REPORT.
 THE SHERBURNE NO,2 AIR QUALITY CONTROL SYSTEM IS IDENTICAL IN DESIGN TO
 THE SYSTEM IN OPERATION ON THE NO.I UNIT  AT THIS STATION.  TWELVE 2.STAGE
 PARTICULATE SCRUBBER (VENTURI-ROD SCRUBBER) AND SULFUR DIOXIDE  ABSORBER
 (MARBLE-BED ABSORBER)  MODULES ARE PROVIDED FOR FLY  ASH AND S02  CONTROL.
 ELEVEN MODULES ARE REQUIRED FOR FULL GENERATING CAPACITY OPERATIONS.
 TOTAL SYSTEM AVAILABILITY  INDEX VALUES REPORTED FOR THE MONTHS  OF  APRIL
 AND MAY WERE 92 AND 91 PERCENT, RESPECTIVELY.
                                                            173
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                                                      BACKGROUND INFORMATION

                                                                ON

                                                 SHERBURNE COUNTY GENERATING PLANT

     THE SHERBURNE COUNTY GENERATING PLANT (SHERCO)  OF THE NORTHERN STATES POWER COMPANY (NSP>  IS LOCATED ON THE MISSISSIPPI

RIVER IN SHERBURNE COUNTY,  BECKER.  MINNESOTA,  APPROXIMATELY *5 MILES NORTHWEST OF MINNEAPOLIS.   THIS NEW POWER-GENERATING PLANT

CURRENTLY HAS TWO COAL-FIRED UNITS  IN SERVICE  AND TWO IN THE EARLY DESIGN STAGES,  UNIT NO.2 IS RATED AT 710 Mw AND FIRES LOW

SULFUR COLSTRlp MONTANA" COAL THAT HAS A HEATING VALUE OF 6300 BTU/LB, SULFUR CONTENT OF 0.8  PERCENT, ASH CONTENT OF 9.0 PERCENTi

AND A MOISTURE CONTENT OF 25.0  PERCENT.  IN ORDER TO MEET MINNESOTA POLLUTION CONTROL AGENCY EMISSION CODES OF 0.96 LB SULFUR

DIOXIDE AND 0.087 LB PARTIcULATES PER MILLION  BTU HEAT-INPUT TO THE BOILER, THE UNIT WAS FITTED WITH A NQN-REGENERABLE LI1ESTONE-

BASED WET SCRUBBING SYSTEM.

     THE DESIGN OF THE SCRUBBER PLANT FOR SHERCO NO.2 IS IDENTICAL TO THAT EMPLOYED FOR THE  NO.l UNIT NOW IN SERVICE AT THIS STA-

TION (SEE THE PRECEDING FILE IN THIS REPORT FOR ADDITIONAL INFORMATION).   THE SCRUBBER DESIGN IS BASED UPON PILOT PLANT AND PROTO-

TYPE PLANT RESEARCH PROGRAMS CONDUCTED AT COMBUSTION-ENGINEERING'S (C-EJ  KREISINGER LABORATORY  AND NSP»S BLACK DOG STATION.  THE

BLACK DOG PROTOTYPE UNIT WAS OPERATED FOR FOURTEEN MONTHS FROM MARCH 1973 TO MAY 197<».  NSP, C-E, AND BLACK ft VEATCH WERE RESPON-

SIBLE FOR THE OPERATION OF THE  13000 ACFH PROTOTYPE SCRUBBER.  THE RESULTS OF THIS PROGRAM INDICATED THAT C-E FIXED-ROD SCRUBBER

AND SINGLE-STAGE MARBLE-BED ABSORBER MODULES WOULD PROVIDE SUFFICIENT POLLUTANT REMOVAL CAPABILITY WITH MINIMAL SCALING AND PLUG-

GING PROBLEMS.  THE SCRUBBING SYSTEM HAS BEEN  GUARANTEED TO REMOVE 99 PERCENT OF THE INLET PARTICULATE MATTER ENTERING THE SCRUB-

BER PLANT OR MAINTAIN AN EMISSION OUTLET OF 0.0* GR/SCF, WHICHEVER VALVE  IS GREATER* AND REMOVE 50 PERCENT OF THE SULFUR IN THE

FUEL (MAXIMUM FUEL SULFUR CONTENT OF 1.2 PERCENT) OR MAINTAIN AN EMMISSION OUTLET OF 200 PPM S02« WHICHEVER VALUE IS GREATER.

     THE SCRUBBER PLANT DESIGN  FOR  SHERCO NO.2 CONSISTS OF 12 C-E VENTRI-ROD SCRUBBER AND MARBLE BED ABSORBER MODULES, 11 OF

WHICH ARE REQUIRED FOR UNIT FULL-LOAD CAPACITY.  EACH MODULE HAS A MAXIMUM FLUE GAS CAPACITY OF 220,000 ACFM AT 135 F.  INCLUDED

IN EACH MODULE IS A VEfjTURI SECTION WITH TWO PARALLEL ROWS OF HORIZONTALLY ORIENTED RODS (PRIMARY CONTACTOR), A SINGLE STAGE

MARBLE-BED (3.5 TO I*.0-INCH DEEP BED OF 13/16-INCH DIAMETER GLASS SPHERES), LADDER VANES FOR GAS-FLOW DISTRIBUTION, TWO-STAGE

CHEVRON-TYPE DEMISTER, FINNED-TUBE  HOT WATER HLAT EXCHANGER, AND AN INTERNAL REACTION TANK.   THE REACTION TANK IS LOCATED AT THE

BOTTOM OF EACH MODULE AND FACILITATES THE COMPLETION OF THE CHEMICAL ABSORPTION OF SOg TO CALCIUM SULFITE.  IN ADDITION,

THE SULFITE SPECIES FORMED IS FORCIBLY OXIDIZED TO SULFATE IN THE REACTION TANK VIA AIR BUBBLING AND AGITATION.  THE SULFATE

SPECIES FORMED IS PRECIPITATED  OUT  BY THE ADDITION OF A GYPSUM SEED TO THE REACTION TANK LIQUOR, DEWATERED IN A 160-FOOT DIAMETER
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SHERBURNE COUNTY (CONTINUED)
CLARIFIERt  AND DISPOSED OF WITH THE COLLECTED PARTICULATE MATTER IN AN ON-SITE Ifl-INCH CLAY-LINED SLUDGE POND (2790  ACRE-FEET

CAPACITY).   WATER is RECYCLED BACK TO THE SCRUBBER PLANT FROM THE DISPOSAL POND FOR  FURTHER SERVICE.

     THE ABSORPTION OF SULFUR DIOXIDE FROM THE FLUE GAS STREAM RESULTS FROM THE PRESENCE  OF TWO ALKALINE MATERIALS.   THE  CALCIUM

OXIDE IN THE COAL FLY ASH (APPROXIMATELY 17 PERCENT BY WEIGHT) AND THE CALCIUM CARBONATE  IN THE TAIL-END LIMESTONE ADDITIVE.

     ADDITIONAL INFORMATION ON THE OPERATION OF THIS UNIT IS PROVIDED IN THE PERFORMANCE  HISTORY TABLE THAT  FOLLOWS.   A SIMPLIFIED

PROCESS FLOW DIAGRAM OF THE SHLRCO SCRUBBER SYSTEM IS PROVIDED IN FIGURE 16« APPENDIX  B.
                                                               175

                                                                                           PEDCo  ENVIRONMENTAL
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                                                          SHERBURNE  NO.  2
              BOILER TIME AND MODULE OPERABILITY (*)
        BOILER
PERIOD    HR.   201  202  203  20"»  205  206  207  208  209   210   211   212

APR. 77   697    0    95   93   67   83   8<»   9«»   7<*   91    87    85    86

TOTAL SYSTEM AVAILABILITY = 92 PERCENT

MEGAWATT-HOURS GENLRATEb = 
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                  TABLE 5
PERFORMANCE DESCRIPTION FOR OPERATIONAL FGD SYSTEMS  06/77
 IDENTIFICATION NO.

 UTILITY NAME

 UNIT NAME

 UNIT LOCATION

 UNIT RATING

 FUEL CHARACTERISTICS

 FGD VENDOR

 PROCESS

 NEW OR RETROFIT

 START UP DATE

 FGD STATUS

 EFFICIENCY,
  PARTICULATES
  79


PENNSYLVANIA POWER CO.


BRUCE MANSFIELD  NO.  1


SHIPPINGPORT PENNSYLVANIA


  635 MW


COAL H.7  PERCENT SULFUR


CHEMICO


LIME SCRUBBING


NEW
 OPERATIONAL
 99.6 PERCENT
  S02
 92 PERCENT GUARANTEE
 WATER MAKE UP
 CLOSED LOOP
 SLUDGE DISPOSAL
  STABILIZED SLUDGE DISPOSED IN  UNLINED POND
 UNIT COST
S133/KW CAPITAL * 2.7 MILLS/KWH ANNUALI2EO
 OPERATIONAL
  EXPERIENCE
 REFER TO THE BACKGROUND INFORMATION SECTION IN TABLE 5 OF THIS REPORT.
 THIS EMISSION CONTROL SYSTEM IS CAPABLE OF REMOVING FLYASH AND S02 FROM
 3.35 MM ACFM OF FLUE GAS VIA WET LIME SCRUBBING.  THE INITIAL SHAKEDOWN
 AND DEBUGGING PHASE OF OPERATION BEGAN FOR PART OF THE SYSTEM IN DECEMBER
 1975. FULL COMMERCIAL OPERATION COMMENCED IN APRIL 1976.  TO OATEt ALL 6
 OF THE SCRUBBING TRAINS HAVE BEEN SUCCESSFULLY PUT INTO OPERATION.
 THE AVAILABILITY INDEX VALUE FOR THE ENTIRE SCRUBBING SYSTEM HAS
 BEEN IN THE MID-90 PERCENT  RANGE SINCE COMMERCIAL START-UP.
                                                            177
                                                                                       PEDCo  ENVIRONMENTAL

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                                                     BACKGROUND INFORMATION

                                                               ON
                                                   BRUCE MANSFIELD UNIT NO. 1
     THE BRUCE MANSFIELD PLANT IS A 2700-Mw, THREE-UNIT, COAL-FIRED FACILITY LOCATED ON THE OHIO RIVER IN THE BOROUGH OF SHIPPING
PORT, PENNSYLVANIA. THIS NEW FACILITY IS BEING BUILT BY PENNSYLVANIA POWER CO., WHICH IS ACTING ON ITS OwN BEHALF AMD AS AGENT FOR
THE OTHER PARTICIPATING COMPANIES* THE CLEVELAND ELECTRIC ILLUMINATING CO., DUOUESNE LIGHT CO., OHIO EDISON CO.. AND TOLEDO EDISON

CO.
     BRUCE MANSFIELD NO. 1 IS A COAL-FIRED, ONCE-THROUGH. SUPERCRITICAL STEAM GENERATOR WHICH FIRES 333 TONS/HR OF COAL GENERATING

APPROXIMATELY 6.5 MM LB/HR OF STEAM AT 3.765 PSIG. 1005 F/1005 F.  THE EMISSION CONTROL EQUIPMENT REQUIRED FOR THIS UNIT IS
DESIGNED TO MEET STATE EMISSION REGULATIONS OF 0.6 LBS SULFUR DIOXIDE/MM BTU OF HEAT INPUT AND 0.0175 GR/SCF OF PARTICULATE WHEN
BURNING 11,900 BTU/LB COAL HAVING AVERAGL ASH AND SULFUR CONTENTS OF 12.5 AND 
-------
                                                        BRUCE MANSFIELD NO.  1
MONTH

DEC. 75

JANt 76
FEB. 76
MAR. 76
APR. 76
          BOILER
                                  OPERATING HOURS
                                    FGU MODULES
506
0     210     96
-------
                                                BRUCE MANSFIE.LD NO, 1 (CONTINUED)
MONTH
BOILER
OPERATING HOURS
  FGD MODULES
      C
                                                                                              COMMENTS
                         A      B        C      D       E

AUG. 76    705.3        672     620     653    535     500

TOTAL SYSTEM AVAILABILITY =  95*

TOTAL SYSTEM OPERABILITY z 100*

TOTAL SYSTEM RELIABILITY a 100*

TOTAL SYSTEM UTILIZATION = 95*

SEP. 76     720         708     617     693    695     596

TOTAL SYSTEM AVAILABILITY =  100*

TOTAL SYSTEM OPERABILITY = 100*

TOTAL SYSTEM RELIABILITY = 100*

TOTAL SYSTEM UTILIZATION = 100*

OCT. 76     739         710    5«»9     631    619     b91

TOTAL SYSTEM AVAILABILITY = 99*

TOTAL SYSTEM OPERABILITY = 100*

TOTAL SYSTEM RELIABILITY s 100*

TOTAL SYSTEM UTILIZATION r 99*

NOV.76      277           270    278     282     113     159

TOTAL SYSTEM AVAILABILITY s 100*

TOTAL SYSTEM OPERABILITY s 100 *

TOTAL SYSTEM RELIABILITY = 100 *

TOTAL SYSTEM UTILIZATION = 38*

DEC. 76     722         58*    726     6B<«    <*33     622

TOTAL SYSTEM AVAILABILITY = 100 *

TOTAL SYSTEM OPERABILITY = 100 *

TOTAL SYSTEM RELIABILITY = 100 *

TOTAL SYSTEM UTILIZATION =975
                                                     F

                                                    668
                                                     691
                                                     2«»6
                                                     626
                                                                180
                                                                                            PEDCo  ENVIRONMENTAL
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                                                BKl/Cf MANSFIELD NO. 1 (CONTINUED)
MONTH
BOILER
OPERATING HOURS
  FGO MODULES
      C      D
                         A     B

JAN. 77     THE UTILITY WAS UNABLE TO PROVIDE

FEB. 77     UPDATE INFORMATION

MAR. 77     FOR THIS REPORT PERIOD.

TOTAL SYSTEM AVAILABILITY = 92 PERCENT

MEGAWATT-HOURS GENERATED = 195,700

APR. 77     PENN POWER REPORTED THAT IT IS

MAY  77     IN THE PROCESS OF REWRITING THE

            BRUCE MANSFIELD NO. 1 FILE FOR

            THE FGD SUMMARY REPORT AND THAT

            IT WILL BE AVAILABLE FOR THE

            NEXT REPORT PERIOD.
                                                                                              COMMENTS
                                                               161
                                                                                           PEDCo  ENVIRONMENTAL
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                  TABLE  5
PERFORMANCE DESCRIPTION  FOR  OPERATIONAL  FcD  SYSTEMS   06/77
 IDENTIFICATION  NO.

 UTILITY  NAME

 UNIT NAME

 UNIT LOCATION

 UNIT RATING

 FUEL CHARACTERISTICS

 FGD VENDOR

 PROCESS

 NEW OR RETROFIT

 START UP DATE

 FGD STATUS

 EFFIClENCYi
  PARTICIPATES
  63


 PHILADELPHIA ELECTRIC  CO.


 EODYSTONE  NO.  IA


 EDDYSTONE  PENNSYLVANIA


  120  MW


 COAL  2.5 PERCENT SULFUR


 UNITED ENGINEERS / PECO


 MAGNESIUM  OXIDE SCRUBBING


 RETROFIT


  9/75


 OPERATIONAL



 99.9  PERCENT
  S02
 90 PERCENT
 WATER MAKE UP
 CLOSED LOOP 1.1 GPM/MW
 SLUDGE DISPOSAL
 UNIT COST
 OPERATIONAL
  EXPERIENCE
S17 MILLION CAPITAL
 REFER TO THE BACKGROUND INFORMATION SECTION IN TABLE 5 OF THIS REPORT.
 THE EMISSION CONTROL SYSTEM FOR THIS UNIT CONSISTS OF THREE PARALLEL
 SCRUBBING TRAINS FOR THE CONTROL OF PARTICULATE AND SULFUH DIOxIDE.
 THE C-SIDE SCRUBBING TRAIN INCLUDES AN S02 ABSORBER MODULE IN SERIES
 WITH A PARTICULATE SCRUBBER. APPROXIMATELY ONE-THIRD OF THE BOILER FLUE
 GAS is SCRUBBED WITH MAGNESIUM OXIDE SLURRY FOR 502 REMOVAL. THE SPENT
 SLURRY is REGENERATED AT THE ESSEX SULFURIC ACID PLANT IN NEWARK. N.J.
 THE REGENERATED MAGOx IS RETURNED TO THE PLANT FOR S02 SCRUBBING SERVICE.
                                                            162
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                                                     BACKGROUND INFORMATION

                                                              ON
                                                        EUDYSTONL NO. 1
     THt EDDYSTONE STATION OF THE PHILADELPHIA ELECTRIC CO. (PECO) IS LOCATED ON THE DELAWARE RIVER IN EDDYSTONE, PENNSYLVANIA,

ABOUT 11 MILES SOUTHWEST OF THE CENTER OF PHILADELPHIA.  THE PLANT IS APPROXIMATELY FIVE MILES WEST OF ONE OF THE MAIN RUNWAYS OF

THE PHILADELPHIA INTERNATIONAL AIRPORT.
     THE STATION HAS FOUR GENERATORS WITH A TOTAL NET GENERATING CAPACITY OF 1370 MW.  UNITS 1 AND 2 BURN COAL WITH AN AVERAGE

GROSS HEATING VALUE OF 12,100 BTU/LB AND ASH AND SULFUR CONTENTS OF 12 PERCENT AND 2.3 PERCENT, RESPECTIVELY, STEAM CONDITIONS ARE

5,000 PSI AND 1150 F.  THESE ARE THE HIGHEST UTILITY PLANT OPERATING PRESSURE AND TEMPERATURE CONDITIONS IN THE UNITED STATES.
UNITS 1 AND 2 ARE BASE-LOAD UNITS.  UNITS 3 AND  SYSTEM ON BOILER NO. i AT THE EDDYSTONE STATION OF PHILADELPHIA

ELECTRIC COMPANY  (PECO) WAS DESIGNED AND INSTALLED BY UNITED ENGINEERS AND CONSTRUCTORS, INC., IN COOPERATION WITH PHILADELPHIA

ELECTRIC.  THE SYSTEM CONSISTS OF THREE FIRST-STAGE SCRUBBER MODULES IN PARALLEL FOR PARTICULATE CONTROL (TWO ENVIRONEERING VENTRI

ROD UNITS AND ONE PEABODY-LURGI VENTURI UNIT) AND A SECOND-STAGE ENVIRONEERING ABSORBER MODULE WITH TWO VENTRI.ROD BEOS FOR SULFUR

DIOXIDE REMOVAL.
     THE THREE FIRST-STAGE SCRUBBERS TOGETHER ARE SIZED TO HANDLE ALL THE EXHAUST GAS FROM UNIT 1 WHICH HAS A NET ELECTRIC GENER-

ATING CAPACITY OF 316 MW.  THE SECOND-STAGE ABSORBER Is SIZED TO HANDLE ONE-THIRD OF THE GAS FLOW, EQUIVALENT TO APPROXIMATELY 105

MU (NET). THE SYSTEM IS DESIGNED TO REMOVE 90 PERCENT OF THE SULFUR DIOXIDE FROM BOILER STACK GAS.  A GENERAL PROCESS FLOW DIAGRAM

OF THE WET SCRUBBING SYSTEM IS PRESENTED IN APPENDIX B.

SCRUBBER OPERATING HISTORY
     THERE WAS A  BRIEF OPERATING PERIOD ON THE PARTICULATE SCRUBBERS FROM MID-NOVEMBER, 1974, TO MARCH, 1975, THAT UNCOVERED A

NUMBER OF PROBLEM AREAS.  DUE TO A NUMBER OF EXTENUATING CIRCUMSTANCES, PARTICULATE SCRUBBING WAS NOT RESTARTED UNTIL JULY 23,
1975. WITH ONE PARTICULATE SCRUBBING TRAIN FOLLOWED BY THE OTHER TWO TRAINS, ON AUGUST 15 AND OCTOBER 2, RESPECTIVELY.  THE SULFUR

DIOXIDE ABSORBER  WAS STARTED FOR THE FIRST TIME ON OCTOBER 2« 1975, AND THE MAGNESIUM OXIDE REGENERATION FACILITY FIRST PROCESSED

MAGNESIUM SULFITE FROM THE EDOYSTONE SCRUBBER ON OCTOBER 26, 1975.


                                                               183

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EDOYSTONE NO.  KCONTINUED)
     THE MAGNESIUM  OXIDE  REGENERATION  FACILITY  HAS  BEEN OPERATED TO PROCESS ALL MAGNESIUM SULFITE MATERIAL SENT TO IT FROM EDDY-
STONE.  THIS OPERATION WAS  USUALLY  ON  A  BATCH BASIS DUE TO THE UPS AND DOWNS AT THE EDOYSTONE SCRUBBER.
     THE SULFUR  DIOXIDE SCRUBBING SYSTEM WAS  TEMPORARILY SHUT  DO*N DECEMBER 31, 1975.  BECAUSE THE ACID PLANT REGENERATION FACILITY
AT THE OLlN CHEMICAL  SULFURIC  ACID  PLANT IN PAULSBORO,  NEW JERSEY PERMANENTLY CEASED OPERATIONS.   THE ACID PLANT REGENERATION
FACILITY WAS RELOCATED TO THE  ESSEX CHEMICAL  PLANT  IN NEWARK*  NEW JERSLY.
     THE PARTICULATE  AND  SULFUR  DIOXIDE  REMOVAL SYSTEM  INSTALLED ON THE EDDYSTONE NO,  1 UNIT Is THE FIRST PHASE OF A TWO-PHAsE
PROJECT.  FOLLOWING SUCCESSFUL DEVELOPMENT OF THIS  SYSTEM WITH MORE CONTINUOUS OPERATION, IT WILL BE INCORPORATED INTO THE DESIGN
FOR THE COMPLETE SULFUR DIOXIDE  REMOVAL  ON EDOYSTONE NO. 2 AND ONE Of THE  TWO EXISTING UNITS AT THE CROMBY STATION.
     ADDITIONAL  INFORMATION AND  DATA CONCERNING THE OPERATION  OF THE PARTICULATE AND SULFUR DIOXIDE SCRUBBERS INSTALLED AT THIS
PLANT ARE PROVIDED  IN THE PERFORMANCE  TABLE.  FOLLOWING.
                                                                                           PEDCo  ENVIRONMENTAL
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                                                     FGO SYSTEM PERFORMANCE
                                                         EDDYSTONE NO.  1
                                                             COMMENTS
NOV. 7»   THE SCRUBBING SYSTEM AT THIS PLANT CONSISTS OF THREE PARALLEL SCRUBBING TRAINS INCORPORATING 3 WET PARTICIPATE SCRUBBERS
DEC. 7»   AND ONE S02 ABSORBER MODULE.  THERE WAS A BRIEF OPERATING PERIOD ON THE PARTICULATE SCRUBBERS FROM MID-NOVEMBER 197"* TO
JAN. 75   MARCH 1975.  PROBLEMS ENCOUNTEKED CENTERED AROUND THE SCRUBBER BOOSTER FANS AND THE FLUE GAS AND LIQUID CONDITIONS.
FEB. 75   THE B-SIOE BOOSTER FAN DEVELOPED HIGH SHAFT VIBRATION WHEN STARTED FOR THE FIRST TIME.  THIS PROBLEM WAS DESIGN-RELATED.
MAR. 75   INVOLVING AN EXCESSIVE CLEARANCE AREA BETWEEN THE SHAFT AND THE WHEEL HUB.  ALSO. EXTENSIVE CORROSION DEVELOPED IN THE
APR. 75   C-SIDE PARTICULATE SCRUBBER INTERNALS.  THIS WAS CAUSED BY LOW SCRUBBING SOLUTION PH LEVELS AND CHLORIDE LEVELS AS HIGH
MAY  75   AS 2000 PPM.  THESE CONDITIONS COUPLED WITH THE THERMAL SHOCK OF A HOT START PROCEDURE CAUSED THE CORROSION.  THIS
JUN. 75   PROBLEM WAS AMELIORATED BY CAUSTIC ADDITION. HIGHER SLOWDOWN AND EMPLOYING A COLD START PROCEDURE.  AT APPROXIMATELY
          THIS TIME. A CHECKOUT OF S02 SYSTEM WAS CONDUCTED.  BLISTERING AND PEELING OF THE POLYURETHANE COATINGS WERE DETECTED
          AND CORRECTED BY RECOATING WITH FLAKE GLASS.
JUL. 75   THE: C-SIDE PARTICULATE SCRUBBER RESTARTED ON JULY 23i 1975.  THE TWO REMAINING TRAINS. B-SIDE AND A-SIDE. WERE PUT INTO
AUG. 75   OPERATION ON AUGUST 15 AND OCTOBER 2. RESPECTIVELY.  THE S02 ABSORBER MODULE IN THE C-SIOE SCRUBBING TRAIN WAS INITIALLY
SEP. 75   PLACED IN SERVICE OCTOBER 2i 1975.  THE OLIN CHEMICAL MGO REGENERATION FACILITY FIRST PROCESSED MAGNESIUM SULFITE FROM
OCT. 75   THE EDDYSTONE SCRUBBER ON OCTOBER 28 • 1975.  THE C-SIDE PARTICULATE SCRUBBER OPERATED A TOTAL OF 2831 HOURS THROUGH
NOV. 75   JANUARY 31. 1976. FOR AN AVAILABILITY OF 70 PERCENT.  THE B-SIDE TRAIN HAS OPERATED A TOTAL OF 1933 HOURS THROUGH
DEC. 75   JANUARY 31. 1976 FOR AN AVAILABILITY OF 55 PERCENT.  THE A-SIDE TRAIN OPERATED A TOTAL OF 626 HOURS THROUGH JANUARY 31.
JAN. 76   1976. FOR AN AVAILABILITY OF 2"* PERCENT.  THE C-SIDE S02 ABSORBER WAS IN SERVICE A TOTAL OF 556 HOURS THROUGH DECEMBER
          31. 1975. WITH AN AVAILABILITY OF 33 PERCENT SINCE STARTUP. PROBLEMS ENCOUNTERED IN THE OPERATION OF THE THREE SCRUBBING
          TRAINS INCLUDED*  UNDER-DESIGNED RECIRCULATION PUMPS. MALFUNCTION OF THE FLUE GAS BY-PASS DAMPER DRIVE UNITS AND
          FAILURE OF THE DOUBLE-BRICK REFRACTORY LINING IN THE REHEAT COMBUSTION CHAMBER.
FEB. 76   OPERATION OF THE S02 SCRUBBING SYSTEM AT EDDYSTONE WAS TEMPORARILY HALTED BECAUSE THE ACID PLANT REGENERATION FACILITY
MAR. 76   AT THE OLIN CHEMICAL SULFURIC ACID PLANT IN PAULSBORO, NEW JERSEY PERMANENTLY CEASED OPERATIONS.  THE UTILITY IS NOW
APR. 76   INVESTIGATING ALTERNATIVE REGENERATION SITES.  A MINIMUM PERIOD OF SIX MONTHS WILL BE REOUIRED FOR RELOCATION ONCE A
                                                               185
                                                                                          PEDCo  ENVIRONMENTAL
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                                              FGD  SYSTEM  PERFORMANCE  (CONTINUED)
                                                       EDDYSTONt  NO.  1
                                                            COMMENTS
MAY  76   CHOICE  IS  HADE.   THE  UTILITY  ANNOUNCED PLANS  FOR  RELOCATION  OF  THE  REGENERATION  FACILITY  AT  THE  ESSEX  CHEMICAL  PLANT  IN
          NEWARK,  NEW  JERSEY.
JUN. 76   RESUMPTION OF  S02 SCRUBBING OPERATIONS IS  PRESENTLY  SCHEDULED FOR DECEMBER  1976.   THE  RELOCATION OF  THE  REGENERATION
JUL. 76   FACILITY IS  NOW  IN PROGRESS.   THE  PARTICULATE SCRUBBERS  ARE  OPERATIONAL.  THE  C-SIDE BOOSTER FAN HAS DEVELOPED  A
AUG. 76   MATERIALS  FAILURE BETWEEN  THE HUB  AND SHAFT  (IDENTICAL TO THE B-SIDE UNIT MENTIONED ABOVEJ.
SEP. 76   ALL  THREE  BOOSTER FANS  HAVE NOW  DEVELOPED  THE MATERIALS  FAILURE BETWEEN THE HUB  AND SHAFT (AS IDENTIFIED IN THE ABOVE
OCT. 76   FOR  THE  B-SIDE UNIT).   THESE  UNITS HAVE  BEEN  RETURNED TO THE MANUFACTURER FOR  MODIFICATIONS  AND  REPAIRS.  CURRENTLY,  ONE
          OF THE PARTIcULATE ScRUBBEKS  IS  IN THE FLUE  GAS STREAM.   TO  DATE, ALL THREE OF THE WET PARTICULATE SCRUBBERS HAVE  NOT
          SEEN ANY APPRECIABLE  SIMULTANEOUS  SERVICE  TIME.
NOV. 76   MGO  SCRUBBING  OPERATIONS ARE  NOW SCHEDULED TO RESTART IN MAY 1977.   REGENERATION FACILITY RELOCATION IS  BEING COM-
DEC. 76   PLETEO,  AND  MODIFICATIONS  TO  THE ID BOOSTER  FANS  CURRENTLY  BEING EFFECTED CONSIST OF CONVERSION  FROM A SHRINK FIT
          TO A SLIP  FIT.  THESE MODIFICATIONS ARE  EXPECTED  TO  ELIMINATE RECURRING VIBRATION PROBLEMS.
JAN. 77   THE  MAGNESIUM  OXIDE  SCRUBBING SYSTEM AT  EDDYSTONE NO. 1A IS  STILL SCHEDULED FOR  RESTART IN MAY 1977.  THE START-UP
FEB. 77   OF THE  NEW MAGNESIUM SULFITE  REGENERATION  FACILITY AT THE ESSEX CHEMICAL PLANT AT NEWARK, N.J. IS ALSO SCHEDULED
MAR. 77   FOR  MAY  1977.   THE THREE PARALLEL  VENTURI  SCRUBBERS  CONTROLLING PARTICULATE EMISSIONS  ON  EDDYSTONE NO. 1 WENT BACK
          INTO SERVICE IN  MARCH 1977.
APR. 77   RESUMPTION OF  MAGNESIUM OXIDE SCRUBBING  OPERATIONS OCCURRED  DURING  THE REPORT  PERIOD.  THE UTILITY REPORTED THAT
MAY 77    S02  SCRUBBING  OPERATIONS WERE NOT  CONTINUOUS  THROUGHOUT  THE  PERIOD. THE ABSORBER WAS IN SERVICE  APPROXIMATELY 206  HOURS
          DURING  MAY.  REGENERATION OPERATIONS AT THE ESSEX  FACILITY WERE  NOT  CONDUCTED DURING THE PERIOD.  PECO INTENDS
          TO INITIATE  S02  RECOVERY AND  MAGOX REGENERATION OPERATIONS DURING THE MONTH OF JuNE. THE  S02 MODULE  CONTAINS TwO
          ABSORBER SECTIONS IN  SERIESCEACH SECTION CONSISTING  OF AN ADJUSTABLE ROD DECK  WITH UNDERSPRA^S). ONLY  ONE OF ABSORBER
          SECTIONS IS  BEING USED  FOR S02 REMOVAL.  S02 REMOVAL  EFFICIENCY  HAS  NOT BEEN MEASURED,  MAGNESIUM  OxIOE  LOSSES IN THE
          SYSTEM  IABSORTION AND REGENERATION)  ARE  ESTIMATED AT 10  PERCENT.
                                                               166
                                                                                     XX  PEDCo  ENVIRONMENTAL
                                                                                                CINCINNATI. OHIO 45246

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                  TABLE 5
PERFORMANCE DESCRIPTION FOR OPERATIONAL FGD SYSTEMS  06/77
 IDENTIFICATION NO.

 UTILITY NAME

 UNIT NAME

 UNIT LOCATION

 UNIT RATING

 FUEL CHARACTERISTICS

 FGD VENDOR

 PROCESS

 NEW OR RETROFIT

 START UP DATE

 FGO STATUS

 EFFICIENCY,
  PARTICULATES
 102

 SPRINGFIELD CITY UTILITIES

 SOUTHWEST NO. 1

 SPRINGFIELD MISSOURI

  200 nw

 COAL 3.5 PERCENT SULFUR

 UNIVERSAL OIL PRODUCTS

 LIMESTONE SCRUBBING

 NEW

  H/77

 OPERATIONAL


 99.7 PERCENT
  S02
 60 PERCENT
 WATER HAKE UP
 SLUDGE DISPOSAL
  STABILIZED SLUDGE DISPOSED IN  UNLINED POND
 UNIT COST
 OPERATIONAL
  EXPERIENCE
S20 MM CAPITAL FOR AQCS
 THE SCRUBBER BLCA«E OPERATIONAL ON A TRIAL BASIS IN EARLY APRIL.  COMMER-
 CIAL OPERATION IS SLATED BY 6/15.  THE SYSTEM IS EXPERIENCING DEMISTER
 SCALING AND SOME CONTROL PROBLEMS.  ALSO CORROSION OF THE PRESATUKATOR
 HAS TAKEN PLACE AND RE-LINING APPEARS NECESSARY.  NO DEFINITE EFFICIENCY
 TESTS HAVE BEEN MADE AS YET DUE TO THE EFFECTS OF THESE PROBLEMS.  THE
 TOP PORTION OF THE STACK AND BREECHING ARE CEILCOTE LINED.
                                                            187
                                                                                       PEDCo  ENVIRONMENTAL
                                                                                              CINCINNATI. OHIO 45246

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                  TABLE 5
PERFORMANCE DESCRIPTION FOR  OPERATIONAL F6D SYSTEMS   06/77
 IDENTIFICATION NO.
 UTILITY NAME
 UNIT NAME
 UNIT LOCATION
 UNIT RATING
 FUEL CHARACTERISTICS
 FGD VENDOR
 PROCESS
 NEW OK  RETROFIT
 START UP  DATE
 FGD STATUS
 EFFICIENCY.
  PARTICULATES

  S02

 WATER MAKE UP

 SLUDGE  DISPOSAL

 UNIT COST
 OPERATIONAL
  EXPERIENCE
103
TENNESSEE VALLEY AUTHORITY
SHAWNEE N0.10A
PADUCAH KENTUCKY
  10 MW
COAL 2.9 PERCENT SULFUR
UNIVERSAL OIL PRODUCTS
LIME/LIMESTONE SCRUBBING
RETROFIT
 «»/72
OPERATIONAL
REFER TO BACKGROUND INFORMATION SECTION IN TABLE 5 OF THIS REPORT. THIS
TURBULENT CONTACT ABSORBER(TCA) LIME/LIMESTONE SCRUBBING SYSTEM HAS BECN
OPERATIONAL SINCE APRIL 1972. THIS TEST PROGRAM IS FUNDtD BY THE EPA.
TVA IS THE CONSTRUCTOR AND FACILITY OPERATOR. THE BECHTEL CORP. OF SAN
FRANCISCO IS THE MAJOR CONTRACTOR. TEST DIRECTOR, AND REPORT WRITER.
                                                            106
                                                                                        PEDCo  ENVIRONMENTAL
                                                                                              CINCINNATI. OHIO 45246

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                  TABLE; s
PERFORMANCE DESCRIPTION FOR OPERATIONAL FGD SYSTEMS  06/77
 IDENTIFICATION NO.
 UTILITY NAME
 UNIT NAME
 UNIT LOCATION
 UNIT RATING
 FUEL CHARACTERISTICS
 FGD VENDOR
 PROCESS
 NEW OR RETROFIT
 START UP DATE
 F60 STATUS
 EFFICIENCY,
  PARTICULATES

  S02

 WATER MAKE UP

 SLUDGE DISPOSAL
 UNIT COST
TENNESSEE VALLLY AUTHORITY
SHAWNEL N0.10B
PADUCAH KENTUCKY
  10 nw
COAL 2.9 PERCENT SULFUR
CHEMICO
LIME/LIMESTONE SCRUBBING
RETROFIT
 «»/72
OPERATIONAL
 OPERATIONAL
  EXPERIENCE
REFER TO BACKGROUND INFORMATION SECTION IN TABLE 5 OF THIS REPORT. THIS
VENTURI/SPRAY TOwER LIME/LIMESTONE SCRUBBING SYSTEM HAS BEEN OPERATIONAL
SINCE APRIL 1972. THIS TEST PROGRAM IS FUNDED BY THE EPA. TVA IS THE
CONSTRUCTOR AND FACILITY OPERATOR. THE BECHTEL CORP. OF SAN FRANCISCO IS
THE MAJOR CONTRACTOR,TEST DIRECTOR, AND REPORT WRITER.
                                                            169
                                                                                        PEDCo  ENVIRONMENTAL
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                                                      BACKGROUND INFORMATION
                                                                ON
                                                      SHAWNEE NOS. IDA AND 10B
     IN JUNE 1968,  THE EPA INITIATED A PROGRAM TO TEST PROTOTYPE LIME AND LIMESTONE SYSTEMS FOR REMOVAL OF SULFUR DIOXIDE AND
PARTICULATE FROM COAL-FIRED BOILER FLUE GASES.  THE PROGRAM MAS CARRIED OUT IN A TEST FACILITY INCORPORATED INTO THE FLUE GAS
DUCTWORK OF UNIT NO. 10. A COAL-FIRED BOILER AT THE TVA SHAWNEE POWER STATION, PADUCAH,  KENTUCKY.   TVA IS THE CONSTRUCTOR AND
FACILITY OPERATOR AND BECHTEL CORP. IS THE MAJOR CONTRACTOR.  TEST DIRECTOR, AND REPORT WRITER.
     THE TEST FACILITY CONSISTS OF THREE PARALLEL SCRUBBER SYSTEMS OF PROTOTYPE SIZE, TREATING PART OF THE FLUE GAS FROM THE
BOILER.  EACH SCRUBBER TRAIN IS CAPABLE OF TREATING APPROXIMATELY 30,000 ACFM OR THE EQUIVALENT OF APPROXIMATELY 10 MW OF POWER
PLANT GENERATING CAPACITY.
     THREE PARALLEL WET SCRUBBER SYSTEMS WERE SELECTED FOR THE TEST PROJECT*  11 A VENTURI WITH A SPRAV TOWER AFTER ABSORBER, 2)  A
TURBULENT CONTACT ABSORBER (TCA), AND 3) A MARBLE-BED ABSORBER.  THE VENTURI SYSTtM, MANUFACTURED BY CHEMICAL CONSTRUCTION CO.,
CONTAINS AN ADJUSTABLE THROAT THAT PERMITS CONTROL AND VARIATION OF PRESSURE DROP UNDER  A WIDE RANGE OF FLOW CONDITIONS.  THE TCA
UNIT, MANUFACTURED  BY UNIVERSAL OIL PRODUCTS, INCORPORATES A  FLU1DIZEO BED OF LOW DENSITY PLASTIC SPHERES THAT ARE FREE TO HOVE
BETWEEN RETAINING GRIDS.  THE MARBLE-BED ABSORBER, SUPPLIED BY COMBUSTION ENGINEERING CO., USES A PACKING OF 3/4-INCH GLASS MARBLE
SPHERES AND A TURBULENT LAYER OF LIQUID AND GAS ABOVE THE MARBLE LAYER TO ENHANCE MASS TRANSFER.
     IN JUNE I97ti  THE EPA BEGAN A 3-YEAR ADVANCED TEST PROGRAM AT THE SHAWNEE FACILITY  WITH THESE MAJOR GOALS*  (1) CONTINUA-
TION OF LONG-TERM TESTING, WITH EMPHASIS PLACED UPON THE RELIABLE OPERATION OF MIST ELIMINATION SYSTEMS AT INCREASED GAS VELOCITY,
(2) INVESTIGATION OF ADVANCED PROCESS AND EQUIPMENT DESIGN VARIATIONS FOR IMPROVING SYSTEM RELIABILITY AND PROCESS ECONOMICS, AND
J3) LONG-TERM RELIABILITY TESTING ON PROMISING PROCESS AND EQUIPMENT DESIGN VARIATIONS.
     THE TWO PARALLEL SCRUBBING SYSTEMS OPERATING DURING THE  ADVANCED PROGRAM ARE THE VENTURI/SPRAY TOWER SYSTEM AND THE TCA UNIT,
GENERAL PROCESS FLOW DIAGRAMS OF THE TWO PROTOTYPE UNITS ARE  PROVIDED IN APPENDIX B.  OPERATION OF THE
MARBLE-BED ABSORBER UNIT HAS BEEN PERMANENTLY DISCONTINUED.
     EACH OF THE SCRUBBING SySTEMS CONTAINS ITS 0«N SLURRY HANDLING FACILITIES AND CAN TREAT APPROXIMATELY 30,000 ACFM OF GAS AT
300 F CONTAINING 1800 TO <*000 PPM OF SULFUR DIOXIDE AND 2 TO  H GRAINS/SCF OF PARTICULATE.  BOILER NO. 1 NORMALLY BURNS A HIGH-
SULFUR BITUMINOUS COAL.
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                                                 SHAWNEE HOS. 10A AND 10B (CONTINUE!))

     FROM JUNE 197«» TO JANUARY 1976, MIST ELIMINATION AND LIMESTONE UTILIZATION TESTS HERE CONDUCTED AT THE SHAWNEE FACILITY.

DURING THIS TEST PERIOD THE VENTURI/SPRA* TOMER SYSTEM WAS OPERATED ON BOTH  LIME AND LIMESTONE AND THE TCA  SYSTEM WITH  LIMESTONE.

TESTING WAS PERFORMED UNDER A CLOSED-WATER-LOOP OPERATION MODE.   DURING THIS PERIOD THE SLURRY SOLIDS CONTAINED APPROXIMATELY  i»0

TO 50 PERCENT-BY-WEIGHT FLY ASH BECAUSE OF RELATIVELY HIGH GAS INLET PARTICULATE LOADING.   THIS TESTING PROGRAn IS SCHEDULED TO

RUN THROUGH TO JUNE 1977.

     ADDITIONAL INFORMATION AND DATA CONCERNING THE DETAILS OF THE ADVANCED  TEST PROGRAM ARE PRESENTED IN THE PERFORMANCE  TABLE

THAT FOLLOWS.
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                                                          SHAWNEE NOS.  IDA AND 10B
SEP. 75     THIS EXPERIMENTAL EPA-FUNDED OPERATION IS PROCEEDING WITH THE TEST PROGRAM,  TWO ABSORBER MODULES ARE CURRENTLY  OPERAT-
OCT. 75     IONAL (10 MW EACH}» THE MARBLE-BED ABSORBER IS STILL INOPEKATIVE (SINCE JULY 1973).   CURRENT EXPERIMENTS ARE RELATED
            TO MIST ELIMINATOR SECTION.
NOV. 75     RECENT TESTING AT SHAWNEE HAS SHOWN THAT THE CHEVRON MIST ELIMINATORS IN BOTH THE SPRAY TOWER AND THE TCA CAN BE KEPT
DEC. 75     FREE OF SOLIDS BUILDUP AT HIGH ALKALI UTILIZATION (GREATER  THAN 90 PERCENT). USING ONLY INTERMITTENT WASHING WITH
            AVAILABLE RAW WATER.  THIS HIGH UTILIZATION IS NORMALLY ACHIEVED WITH LIME*  IT HAS BEEN ACHIEVED WITH LIMESTONE AT  RE-
            DUCED SCRUBBER INLET SLURRY  PH (ABOUT 5.21  AND WITH THREE EFFLUENT TANKS IN  SERIES TO SIMULATE A PLUG-FLOW REACTOR.
            TESTING IS CONTINUING TO DETERMINE THE EFFECTS OF PROCESS VARIABLES ON MIST  ELIMINATOR PERFORMANCE AND ON LIMESTONE
            UTILIZATION. FUTURE PLANS INCLUDE*  (1)  FACTORIAL TESTING WITH LIME AND LIMESTONE TO DETERMINE THE EFFECTS OF PROCESS
            VARIABLES ON S02 REMOVAL AND (2)  TESTING THE OXIDATION OF SLUDGE TO GYPSUM IN THE VENTURI/SPRAY TOWER SYSTEM USING  AIR
            SPARGING OF AN ACIDIFIED SLURRY BLEED STREAM.
JAN. 76     THE ADVANCED TEST PROGRAM IS CONTINUING.  HIGHLIGHTS OF THE PROGRAM ARE AS FOLLOWS*
FEB. 76         EVALUATE SCRUBBER OPERABILITy DURING VARIABLE LOAD OPERATION.
                CONTINUE LONG-TERM RELIABILITY TESTING.
                INVESTIGATE METHODS FOR  IMPROVING WASTE SOLIDS SEPERATION.
                CONTINUE SLUDGE OXIDATION AND SLUDGE FIXATION STUDY PROGRAMS.
                EVALUATE SYSTEM PERFORMANCE AT REDUCED FLY ASH LOADINGS.
                DETERMINE THE PRACTICAL UPPER LIMITS OF SOg REMOVAL EFFICIENCY.
                EVALUATE ADDITION OF MAGNESIUM ION TO THE SCRUBBING SLURHY.
                CHARACTERIZE ALL STACK GAS EMISSION COMPONENTS.
                EVALUATE MATERIALS OF CONSTRUCTION OF ALL SCRUBBER AND PLANT-RELATED COMPONENTS.
                DEVELOP A COMPUTER PROGRAM FOR DESIGN AND COST ANALYSIS OF FULL-SCALE LIME/LIMESTONE SYSTEM.
MAR. 76     BECHTEL REPORTED THAT THE FACTORIAL TEST PROGRAM, EVALUATING THE PERFORMANCE OF THE LIME/LIMESTONE SCRUBBING
APR. 76     SYSTEMS WITH AND WITHOUT MAGNESIUM ADDITION HAS BEEN COMPLETED.  CURRENTLY TESTING IS PROCEEDING ON THE EVALUATION
            OF SYSTEM PERFORMANCE AS A FUNCTION OF LOW RESIDENCE TIMES  (1.5 TO 5.0 MINUTESj IN THE RECYCLE TANKS.  IN ADDITION,
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                                                         NOS. IDA AND 108  (CONTINUED)
                A FLY ASH-FREE DUCT IS BEING INSTALLED AT THE TEST FACILITY. THUS ENABLING EVALUATION OF SYSTEM PERFORMANCE IN
                THE ABSENCE OF FLY ASH,
HAY  76         THE TEST DIRECTOR, BECHTEL, PROVIDED THE FOLLOWING INPUT CONCERNING THE OPERATION OF THE EXPERIMENTAL SCRUBBING
JUN. 76         SYSTEMS DURING THE REPORT PERIOD*
                     THE EFFECT OF MGO AUDITION WAS EXPLORED IN BOTH SCRUBBER SYSTEMS.  RESULTS INDICATE MAGNESIUM ION IN THE
                     SCRUBBER SLURRY LIQUOR ENHANCES SOg REMOVAL AND CAN DEPRESS SULFATE SUPERSATURATION.  IT WAS FOUND THAT THE
                     MAGNESIUM ION CONCENTRATION HAD TO EXCEED THE EQUIVALENT CHLORIDE ION CONCENTRATION TO HAVE AN EFFECT ON S02
                     REMOVAL.
                     IN THE TCA UNIT, WITH LIMESTONE SLURRY• S02 REMOVAL WAS INCREASED FROM 75 TO 93 PERCENT BY INCREASING THE
                     MAGNESIUM ION CONCENTRATION TO 9.000 PPM IN EXCESS OF EQUIVALENT CHLORIDE ION.  TO ACHIEVE THIS CONCENTRATION
                     LEVEL, MAGNESIUM OXIDE WAS ADDED AT A RATE EQUAL TO 6 PERCENT BY WEIGHT OF THE LIMESTONE ADDITION RATE.
                     IN THE VENTURI/SPRAY TOWER SYSTEMS, WITH LIME SLURRY, S02 REMOVAL WAS INCREASED FROM 75 TO 90 PERCENT BY IN-
                     CREASING MAGNESIUM  ION CONCENTRATION TO 2,000 PPM IN EXCESS OF EQUIVALENT CHLORIDE ION.  THE MAGNESIUM OXIDE
                     ADDITION RATE WAS 2 PERCENT BY WEIGHT OF THE LIME ADDITION RATE.
                     BOTH SCRUBBING SYSTEMS OPERATED IN THE SUBSATURATED SULFATE MODE WHEN MAGNESIUM OXIoE WAS ADDED.  INLET S02
                     CONCENTRATIONS DURING THE TESTS AVERAGE APPROXIMATELY 3.000 PPM DURING THESE TESTS.
                     FOLLOWING THE TEST BLOCKS MENTIONED ABOVE, BOTH SCRUBBERS ARE OPERATING UITH LIME SLURRY SCRUBBING SOLUTIONS,
                     THE TCA SYSTEM ON FLUE GAS CONTAINING FLY ASH AND THE VENTURI/SPRAY TOWER SYSTEM ON FLY ASH-FR£E FLUE GAS.
JUL. 76         EXPERIMENTAL OPERATION OF THE EPA/TVA ALKALI SCRUBBING TEST FACILITY CONTINUED DURING THE REPORT PERIOD.  BECHTEL.
AUG. 76         THE TEST DIRECTOR, PROVIDED THE FOLLOWING INPUT CONCERNING THE OPERATION OF THE PROTOTYPE TEST UNITS.
                    VENTURI/SPRAY TOWER SYSTEM* THIS SYSTEM RAN ON FLY ASH.FREE FLUE GAS USING A LIME SLURRY SCRUBBING SOLUTION.
                    NO SIGNIFICANT DIFFERENCES IN 502 REMOVAL. GYPSUM SATURATION AND SULFITE OXIDATION WERE DETECTED (VERSUS FLY
                    ASH-LADEN FLUE GAS}.  ONE DIFFERENCE NOTED WAS THE FILTER CAKE SOLIDS CONTENT WHICH WAS APPROXIMATELY 10 PER-
                    CENT LOWER FOR THE FLY ASH-FREE SLUDGE O»0 TO 50 PERCENT SOLIDS) VERSUS THE FLY ASH-LADEN SLUDGE (50 TO 60
                    PERCENT SOLIDS).  IN ADDITION, OPERATION IN A LOw RESIDENCE TIME MODE (3 MINUTES) WAS EXPLORED.  SCALE-FREE
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                                                 SHAWNEE  NOS.  IDA  AND  10B  (CONTINUED)
                    OPERATION  WAS  ACHIEVED  IN  THIS  MODE. UNDER  THE  FOLLOWING  CONDITIONS*   8  PERCENT  SOLIDS  (NO FLY  ASH)  IN  THE RE-
                    CIRCULATED SLURRY*  PH OF THE  SCRUBBER LIQUID  INLET WAS 6.0*  SUPERFICIAL GAS  VELOCITY OF  9.<»  FT./SEC.*  AND A
                    TOTAL LIOUIO-TO-GAS RATIO  (L/G)  OF 7! GAL./MCF.  SOME  SCALE  FORMATION OCCURRED  WHEN THE  SOLIDS CONTENT  IN THE
                    RECIRCULATED SLURRY DROPPED BELOW THE 
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                                                         NOS. 104 /.   138 (CONTINUED)

                AND THERE APPEARS TO BE AN OPTIMIM RESIDENCE: TIME AT WHICH MINIMUM SULFATE (GTPSUM)  SUBSATURATiON OCCURS.   TYPICAL

                CONDITIONS* GAS VELOCITY 12.5 FT/SEC,  L/G OF 50.  PH OF 7.0,  2000  PPM OF  MG ION,  AND  6 PERCENT SOLIDS.   AT  THESE

                CONDITIONS GYPSUM SATURATIONS WERE 95.  50,  AND 92 PERCENT, AT RESIDENCE  TIMES OF 3.  4,  AND 12 MINUTES,  RESPECTIVE-

                LY.  FURTHER TESTS WERE RUN AT 37 GAL/hCF L/G, AND 8.0 SCRUBBER INLET PH WITH OTHER  CONDITIONS THE SAME.   DURING

                THESE TESTS GTPSUM SATURATIONS WERE 95t 95. 50.  AND 90 PERCENT AT 3, <»»  5.It  AND 16  MINUTES RESIDENCE  TIMES.

                RESPECTIVELY.

NOV. 76         FROM MID-OCTOBER THROUGH EARLY DECEMBER AN INTENSIVE FLUE GAS CHARACTERIZATION TESTING PROGRAM WAS CONDUCTED  ON

DEC. 76         THE VENTURI/SPRAY TOWER SYSTEM WITH LIME SLURRY.

                OVER THE RANGE TESTED, OUTLET PARTICULATE MASS LOADING WAS FOUND TO BE INDEPENDENT OF SLURRY COMPOSITION  (8 TO 15

                PERCENT SUSPENDED SOLIDS, 3,000 TO 16,000 PPM DISSOLVED SOLIDS),  GAS FLOW RATE (20,000 To 35,000 ACFM), SPRAY

                TOWER LIQUID RATE (0 TO 1,400 6PM), AND VENTURI PRESSURE DROP (3 TO 9 INCHES H20).  WITH H TO 6 GR/OSCF PARTICU-

                LATE IN THE INLET, TYPICAL OUTLET LOADINGS WERE 0.02 TO O.Oi* GR/OSCF.  WHEN OPERATING WITH FLUE GAS FROM  THE

                ELECTROSTATIC PRECIPITATOR (0.1 TO O.t GR/DSCF TO THE SCRUBBER),  THE SCRUBBER OUTLET LOADING AVERAGED  0.005

                GR/OSCF.  THUS, ENTRAINED SLURRY FROM THE MIST ELIMINATOR MUST HAVE BEEN LESS THAN 0.005 GR/DSCF.  SIZE DISTRIBU-

                TION DATA ARE STILL BEING ANALYZED.  SULFURIC ACID MIST VALUES WERE APPROXIMATELY 2 TO 25 PP« AT THE SCRUBBER IN-

                LET AND REMOVALS HAVE BEEN ABOUT 50 TO 75 PERCENT.

                FOR THE REMAINDER OF DECEMBER THE VENTURl/SPRAY TOWER SYSTEM WAS DOWN FOR MODIFICATIONS FOR TWO-STAGE  OXIDATION

                TESTING.  SEE APPENDIX B FOR A PROCESS FLOW DIAGRAM.

                DURING NOVEMBER THE TCA WAS OPERATED WITH FLY-ASH CONTAINING FLUE GAS USING LIME SLURRY WITHOUT ADDED  MAGNESIUM

                OXIDE.  OPERATING CONDITIONS WERE 12.5 FT/SEC GAS VELOCITY, 50 GAL/MCF L/G, 6.0 SCRUBBER INLET PH, AND 8  TO 15

                PERCENT SLURRY SOLIDS.  AT THESE CONDITIONS THE S02 REMOVAL WAS ABOUT 80 PERCENT.

                FLY-ASH FREE LIMESTONE TESTS WITHOUT MAGNESIUM OXIDE ADDITION BEGAN ON THE TCA SYSTEM IN LATE NOVEMBER.  TYPI-

                CAL OPERATING CONDITIONS WERE 12.5 FT/SEC GAS VELOCITY. 50 GAL/MCF L/G,  AND 1.1 TO 1.2 STOICHIOMETRIC  RATIO.  AT

                THE SAME STOICHIOMETRY, THE PH OF THE FLY-ASH FREE SLURRY WAS 0.2 TO 0.3 UNITS HIGHER THAN OBSERVED IN PREVIOUS

                RUNS WITH FLY ASH.
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                                                SHAWNEE NOS.  IDA AND  108  (CONTINUED)
JAN. 77         THE  VENTURI/SPRAY  TOWER  SYSTEM HAS BEEN OPERATED  IN A  TWO-SERIES-SCRUBBER MODE  WITH FORCED OXIDATION  SINCE EARLY
FEB. 77         JANUARY  1977  AFTER  SYSTEM  MODIFICATIONS TO  ALLOW  OPERATION  OF  THE  VENTURI AND SPRAY TOWER WITH  INDEPENDENT SLURRY
                RECIRCULATION LOOPS.   SULFITE OXIDATION WAS CARRIED OUT  IN  AN  e  FT. DIAMETER VENTURI  CPRE-SCRUBBER) EFFLUENT HOLD
                TANK WHICH  HAD A 130  - 1/8 INCH HOLE  AIR SPARGER  IMMERSED  IN 18  FT. OF  SLURRY.   THE SPRAY TOWER  (AFTER  SCRUBBER)
                FUNCTIONED  AS A PRIMARY  S02  ABSORBER.
                TYPICAL  OPERATING  CONDITIONS. USING LIMESTONE  SLURRY,  WERE  6.7 FT/SEC SPRAY TOWER GAS VELOCITY,  20-30 6AL/MCF
                VENTURI  L/G,  70 GAL/MCF  SPRAY TOWER L/G. 15 PERCENT SOLIDS  (WITH FLY ASH) IN VENTURI  RECIRCULATED  SLURRY. 4.5-5.0
                VENTURI  INLET (OXIDATION TANK) PH, AND 11.3 MINUTES OXIDATION  TANK RESIDENCE TIME (BASED ON  600  GPM SLURRY FLOW TO
                VENTURI).
                DURING THESE  TESTS,  AVERAGE  OVERALL SULFITE OXIDATION  RANGED FROM  93 TO 99 PERCENT AT AIR STOICHIOMETRIC  RATIO OF
                1.0  TO i».7  LB-ATOMS OXYGEN/LB-MOLE S02 ABSORBED.  CORRESPONDING  AVERAGE OXIDATION IN  THE SPRAY  TOWER  RANGED FROM
                10 TO 16 PERCENT.   AVERAGE OVERALL LIMESTONE UTILIZATION RANGED  FROM 83 TO 96 PERCENT.  NO SCALING JAS  EXPERIENCED
                IN EITHER SCRUBBER.   AVERAGE FILTER CAKE SOLIDS WERE 79  TO  86  PERCENT BY WEIGHT COMPARED WITH 55-65 PERCENT WITH-
                OUT  FORCED  OXIDATION.  SLURRY SOLIDS  SETTLING  RATE RANGED  0.5  TO l.H CM/MIN. 5  TO 10  TIMES FASTER  THAN  THAT FOR
                UNOXIDIZED  SLURRY.   FINAL  SETTLED DENSITY RANGED  65-80 PERCENT SOLIDS COMPARED  WITH if5-60 PERCENT  FOR SLURRY WITH-
                OUT  FORCED  OXIDATION.
                FLY  ASH-FREE  LIMESTONE TESTING ON THE TCA SYSTEM  WAS COMPLETED IN  EARLY FEBRUARY.  THE  PH OF THE FLY  ASH-FREE
                SLURRY WAS  0,2 TO  0.3  UNITS  HIGHER THAN OBSERVED  IN PREVIOUS RUNS  WITH  FLY ASH.  IN ADDITION, THE  FLY ASH-FREE
                SLURRY APPEARED TO HAVE  INFERIOR SOLIDS OEWATERING CHARACTERISTICS.  FOR EXAMPLE, THE CENTRIFUGE CAKE SOLIDS
                AVERAGED ABOUT 50  PERCENT  COMPARED WjTH ABOUT  60  PERCENT FOR SLUDGE CONTAINING  FLY ASH.
                INTENSIVE FLUE GAS CHARACTERIZATION TESTING WITH  LIMESTONE  SLURRY  ON THE TCA SYSTEM BEGAN IN EARLY FEBRUARY AND
                ENDED IN EARLY MARCH  1977.  PRELIMINARY ANALYSIS  OF THE  DATA SHOWED AN  OUTLET MASS LOADING OF o.oi-o.OB GRAIN/DSCF
                FOR  FLUE GAS  CONTAINING  FLY  ASH AND 0.02-0.03  GRAlNS/DSCF  FOR  FLUE GAS  WITHDRAWN DOWNSTREAM  OF  THE ESP.  IT WAS
                ESTIMATED THAT THESE  OUTLET  MASS LOADINGS CONTAINED ABOUT  0.03 GRAIN/DSCF FLY ASH, 0.02 GRAIN/DSCF RE-ENTRAINED
                SLURRY SOLIDS, AND 0.015 ENTRAINED DISSOLVED SOLIDS (WHEN  A CONTINUOUS  MIST ELIMINATOR  UNDER WASH  WAS USED). THESE
                VALUES VARY DEPENDING ON THE MIST ELIMINATOR WASH SCHEME AND GAS FLOW RATE.

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                                                 SHAWNEE NOS. 10A AND 10B (CONTINUED)
MAR. 77         DURING MARCH,  THE VENTURI/SPRAY TOWER  t»AS TESTED WITH LIME SLURRY AND FLY ASH LADEN FLUE GAS IN A TWO-STAGE SCRUB-
                BER NODE WITH  FORCED OXIDATION. OPERATION WITH LIME WAS SIMILAR TO THE PREVIOUSLY REPORTED LIMESTONE  OPERATION
                WITH GREATER THIN 95 PERCENT OXIDATION AT AN AIR STOICHIOMETRIC RATIO OF 1.5 LB-ATOMS OXYGEN/LB-MOLE  S02  ABSORBED
                WITH A SIMPLE  AIR SPARGER IN A VENTURI HOLD TANK.  SLURRY SOLIDS SETTLING RATE VARIED FROM 0.6 TO 1.3 CM/MIN (A 5
                TO 10 FOLD ENHANCEMENT OVER UNOXIDIZED SLURRY) AND FILTER CAKE SOLIDS RANGED FROM 7t TO 86 PERCENT (COMPARED WITH
                <*5 TO 60 PERCENT WITH UNOXIDIZED SLURRY).
                TWO MAJOR DIFFERENCES BETWEEN LIME AND LIMESTONE WERE OBSERVED IN A TWO-STAGE FORCED OXIDATION.  TO MAINTAIN PH
                CONTROL, IT WAS NECESSARY TO FEED LIME TO BOTH STAGES. WITH LIMESTONE, FEED ONLY TO THE SECOND STAGE  WAS  ADEQUATE.
                TO MAINTAIN 80 PERCENT S02 REMOVALt IT WAS NECESSARY TO OPERATE WITH HIGHER SLURRY SOLIDS CONCENTRATION IN THE
                SPRAY TOWER LOOP WITH LIMESTONE (15 PERCENT) THAN WITH LIME (6 PERCENT), RESULTING IN A TIGHTER WATER BALANCE WITH
                LIMESTONE AND INADEQUATE WATER TO FLUSH THE MIST ELIMINATOR.
                PRELIMINARY LIMESTONE TYPE AND GRIND TESTS MADE ON THE TCA SYSTEM DURING MARCH INDICATED THAT S02 REMOVAL IS
                IMPROVED BY THE USE OF FINER GROUND LIMESTONE.  S02 REMOVAL WITH EQUIVALENT GROUND FREDONlA WHITE AND LONGVlEW,
                ALABAMA LIMESTONES WAS THE SANE.
                BLEEDSTREAM FORCED OXIDATION TESTS ARE BEING CONDUCTED WITH A PENBERTHY ELL-3 EJECTOR IN A CLOSED LOOP AROUND A
                BLEED STREAM HOLD TANK. INITIAL TESTS  WERE UNSUCCESSFUL DUE TO HIGH PH OF 7 TO 8 IN THE HOLD TANK.  BY LOWERING
                THE HOLD TANK PH TO 5 TO 6, SULFITE,OXIDATION UP TO 96 PERCENT WAS ACHIEVED.
APR. 77         UNIT 10 BOILER WAS SHUT DOWN FOR A SCHEDULED TWO-MONTH MAINTAINANCE OUTAGE.  BECAUSE OF THE BOILER OUTAGE, THE
MAY. 77         SHAWNEE SCRUBBERS WILL NOT OPERATE DURING APRIL AND MAY.
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                  TABLE  5
PERFORMANCE DESCRIPTION  FOR  OPERATIONAL  FGO SYSTEMS   06/77
 IDENTIFICATION NO.
 UTILITY NAME
 UNIT NAME
 UNIT LOCATION
 UNIT RATING
 FUEL CHARACTERISTICS
 FGD VENDOR
 PROCESS
 NEW OR  RETROFIT
 START UP DATE
 FGO STATUS
 EFFICIENCYt
  PARTICULATES
 105
 TENNESSEE VALLEY AUTHORITY
 WIDOWS CREEK NO. 6
 BRIDGEPORT ALABAMA
  550 MW
 COAL   3.7 PERCENT SULFUR
 TENNESSEE VALLEY AUTHORITY
 LIMESTONE SCRUBBING
 RETROFIT
  5/77
 OPERATIONAL

 99.5 PERCENT
  S02
 80 PERCENT
 WATER  MAKE  UP
 SLUDGE  DISPOSAL
 UNSTABILIZEO SLUQGE DISPOSED IN UNLINED POND
 UNIT  COST
S102/KW CAPITAL*!.72 MILLS/   KWH OPERATING
 OPERATIONAL
  EXPERIENCE
 REFER TO THE BACKGROUND INFORMATION SECTION IN TABLE s OF THIS REPORT.
 THE EMISSION CONTROL SYSTEM FOR THIS 550-HW COAL-FIRED POWER-GENERATING
 UNIT CONSISTS OF EXISTING ELECTROSTATIC PREClPITATOHS FOLLOWED BY FOUR
 PARALLEL SCRUBBING TRAINS, EACH CAPABLE. OF HANDLING 25 PERCENT OF THE
 BOILER FLUE GAS FROM UNIT NO. 8. INITIAL OPERATION OF THE SCRUBBER PLANT
 OCCURRED ON MAY 16. FLUE GAS WAS PASSED THROUGH TWO (TRAINS A AND B) OF
 THE *> TRAINS. FLUSHING AND CLEANOUT OF THE REMAINING 2 TRAINS IS STILL IN
 PROGRESS. BOILLR CAPACITY WAS APPROXIMATELY 50 PERCENT OF FULL LOAD.
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                                                      BACKGROUND INFORMATION
                                                                ON
                                                        WIDOWS CREEK NO. 8
     IN MID-1970. TENNESSEE VALLEY AUTHORITY DECIDED TO INSTALL A FULL-SCALE DEMONSTRATION LIMESTONE SCRUBBING S02 REMOVAL SYSTEM
ON GENERATING UNIT NO. 8 AT THE WIDOWS C«EEK PLANT.  THE PRIMARY OBJECTIVE WAS TO WORK OUT DESIGN AND OPERATING PROBLEMS IN S02
REMOVAL OPERATIONS AS A PREPARATION FOR THE POSSIBILITY OF FUTURE TVA FGD OPERATIONS.
     THE WIDOWS CREEK POWER STATION IS LOCATED IN NORTHEAST ALABAMA, NEAR CHATTANOOGA, TENNESSEE.  UNIT NO. 8 IS A COAL-FIRED
BOILER WITH A MAXIMUM GENERATING CAPACITY OF 550 MW, AND A MAXIMUM STACK GAS RATE OF 1,600,000 CFM AT 280 DEGREES F.  THE BOILER
AND ESP UNITS WERE COMMISSIONED BY TVA IN 1963.
     THE UET LIMESTONE FGD SYSTEM AT WIDOWS CREEK WAS PLACED IN SERVICE ON MAY Ifc, 1977. THE SYSTEM CONSISTS OF FOUR IDENTICAL
SCRUBBING MODULES (IDENTIFIED AS A, B, C» AND 0) EACH HANDLING 25 PERCENT OF THE FLUE GAS FROM UNIT NO. 8. LIMESTONE STORAGE AND
MILLING FACILITIES AND A SLUDGE DISPOSAL POND ARE ALSO LOCATED ON SITE.
     FLUE GAS ENTERING THE SCRUBBING MODULE FROM THE EXISTING ELECTROSTATIC PRECIPITATORS PASSES THROUGH A HOO.OOO ACFM CAPACITY

F.D. FAN AND INTO THE VENTURI. THE VENTUKI SCRUBBER IS A RECTANGULAR THROAT DESIGN USED TO SATURATE, AND REMOVE FLYASH
FROM THE GAS. DUE TO THE INEFFICIENCY OF THE OLD ESP UNITS, LARGE VENTuRI SCRUBBERS WERE REQUIRED IN ALL MODULES TO REMOVE PARTI-
CULATES. S02 REMOVAL EFFICIENCY IN THE VENTURI IS ABOUT 10 PERCENT.  THE ABSORBER IS A GRID TYPE ABSORPTION TOWER WHICH WAS
SUPPLIED BY POLYGON.  THE GRID TOWER WILL BE USED INITIALLY AS A SPRAY TOWER AND WILL OPERATE AT A LlOUlD-TO-GAS RATIO OF 50.
THE S02 REMOVAL EFFICIENCY FOR THE ABSORBER IS ABOUT 70*, GIVING A COMBINED SCRUBBER DESIGN EFFICIENCY OF ABOUT 80 PERCENT FOR
THE ABSORBER AND VENTURI TOGETHER.  THE ENTRAPMENT SEPARATOR IS A CHEVRON VANE TYPE (4 PASS) LOCATED VERTICALLY IN A HORIZONTAL
SHELL.  THE REHEAT SYSTEM CONSISTS OF A STEAM/HOT AIR INJECTION SYSTEM RAISING THE FLUE GAS TO AN OUTLET TEMPERATURE OF 175F.
     LIMESTONE HANDLING AND MILLING EQUIPMENT INCLUDES A SHAKER FOR TRUCK AND RAIL UNLOADING, A LIVE STORAGE SILO, A WET BALL
MILL, AND A CYCLONE CLASSIFIER. THE GRINDING SySTEM IS DESIGNED TO PRODUCE A GROUND PARTICLE SIZE OF 90 PERCENT MINUS 200 MESH.
AT THE DESIGN RATE OF 50 TONS PER HOUR DRY LIMESTONE.  THE UNLOADING AND STORAGE FACILITIES UP TO AND INCLUDING THE LIVE STORAGE
SILO ARE DESIGNED TO ACCOMODATE A FUTURE LIMESTONE SCRUBBING FACILITY ON WIDOWS CREEK UNIT NO. 7.
     WASTE BY-PRODUCT SOLIDS FROM THE SCRUBBING FACILITY WILL BE DISPOSED OF IN A DIKED POND 100 ACRES IN AREA BY 30 FEET IN
HEIGHT.  AN ADDITIONAL 10 FEET IN HEIGHT MAY BE ADDED TO YIELD A TOTAL SLUDGE STORAGE CAPACITY OF 5.8 MM. CUBIC YARDS, OR 10 YEARS
OF SCRUBBER EFFLUENT STORAGE.  THE SLUDGE, CONSISTING OF FLYASH, REACTION PRODUCTS (HYDRATES OF CALCIUM SULFITE AND SULFATE) AND


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WIDOWS CREEK NO.  8 (CONTINUED)

UNREACTED LIMESTONE IS PUMPED  TO  THE  PONU  AS  A  15-16  PERCENT  SOLIDS  SOLUTION.

     THE WIDOWS CREEK  NO.  a SCRUBBING UNIT IS DESIGNED  TO  BE  AS  FLEXIBLE  AS  POSSIBLE.  A  LARGE  RESERVOIR  OF  QUENCH WATER  IS  LOCATED

ABOVE THE ABSORBER TO  GRAVITY  FEED  WATER TO THE TOWER IN CASE OF POWER  FAlLUREt  THEREBY  SAVING THE  ABSORBER AND RUBBER LINING.

THE ABSORBER CAN  BE OPERATED AS A MULTI-GRID, TURBULENT CONTACT, OR  SPRAY TOWER  ABSORBER.  PROVISIONS  HAVE BEEN HADE  IN THE

ABSORBER DESIGN SO THAT IT CAN READILY BE  CONVERTED  TO  A MOBILE  BED  TYPE  ABSORBER  SHOULD IT  PROVE DESIRABLE IN THE FUTURE TO

OBTAIN IMPROVED S02 REMOVAL.  REFER TO APPENDIX B  FOR A PROCESS  FLOW DIAGRAM.
                                                               200
                                                                                /X~^\
                                                                                          PEDCo  ENVIRONMENTAL
                                                                                                 CINCINNATI. OHIO 45246

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            TABLE  6

NUMBER AND TOTAL MW OF FGD SYSTEMS
                  201
                                     PEDCo  ENVIRONMENTAL
                                           CINCINNATI. OHIO 45246

-------
202
                        PEDCo ENVIRONMENTAL
                              CINCINNATI. OHIO 45246

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               TABLE fa
NUMBER AND TOTAL WW OF FGD SYSTEMS
      STATUS




   OPERATIONAL

   UNDER CONSTRUCTION

   PLANNING
     CONTRACT AWARDED
                          NO.OF
                          UNITS
                             27

                             29
                             20

LETTER OF INTENT              5

REQUESTING/EVALUATING BIDS    5

CONSIDERING ONLY FGD SYSTEMS 33

TOTAL                       119
                                     MW
 7819.
 9797.

 1892.

 3565.

1*656.

50577.
                                                      203
                                                                                  PEDCo  ENVIRONMENTAL
                                                                                        CINCINNATI. OHIO 45246

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20<*
                          PEDCo  ENVIRONMENTAL
                                CINCINNATI. OHIO -45246

-------
            TABLE  7

SUMMARY OF F6D SYSTEMS BY COMPANY
                 205
                                    PEDCo  ENVIRONMENTAL
                                          CINCINNATI. OHIO 45246

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206
                        PEDCo  ENVIRONMENTAL
                             CINCINNATI. OHIO 45246

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                                         TABLE  7
                                SUMMARY OF  FGO  SYSTCMS BY  COMPANY
         UTILITY

ALABAMA ELECTRIC COOP
ALLEGHENY POWER SYSTEM
ARIZONA ELECTRIC POWER COOP
ARIZONA PUBLIC SERVICE
BASIN ELECTRIC POWER COOP
BIG RIVERS ELECTRIC COOP CORP.
BRAZOS ELECTRIC POWER COOP
CENTRAL ILLINOIS LIGHT CO.
CENTRAL ILLINOIS PUBLIC SERV
CINCINNATI GAS > ELECTRIC CO.
COLORADO UTE ELECTRIC ASSN.
COLUMBUS ft SOUTHERN OHIO ELEC.
COMMONWEALTH EDISON
DUOUESNE LIGHT
EASTERN KENTUCKY POWER COOP
INDIANAPOLIS POWER ft  LIGHT CO.
KANSAS CITY POWER ft LIGHT
KANSAS POWER ft  LIGHT
KENTUCKY UTILITIES
LOUISVILLE GAS  I ELECTRIC
MINNESOTA POWER AND LIGHT  CO.
MINNKOTA POWER  COOPERATIVE
MONTANA  POWER  CO.
NEVADA POWER
NEW ENGLAND ELEC SYSTEM
NIAGARA  MOHAWK  POWER  COOP.
NORTHERN INDIANA PUB  SERVICE
NORTHERN STATES POWER CO.
OTTER TAIL POWER COMPANY
PACIFIC  POWER  AND LIGHT  CO.
PENNSYLVANIA POWER  CO.
PHILADELPHIA ELECTRIC CO.
POTOMAC  ELECTRIC *  POWER
PUBLIC  SERVICE  CO OF  NEW  MEx.
PUBLIC  SERVICE  OF  INDIANA
SALT RIVER PROJECT
SOUTH CAROLINA  PUBLIC SERVICE
SOUTHERN  ILLINOIS POWER  CO OP
SOUTHERN  INDIANA GASSELECTRIC
SOUTHERN MISSISSIPPI  ELECTRIC
SPRINGFIELD CITY UTILITIES
TENNESSEE. VALLEY AUTHORITY
TEXAS POWER &  LIGHT CO.
TEXAS POWER AND LIGHT CO.
TftT Al
TUT AL
flDCO AT TAMAI
V/rl_KA| lUrVAC



CONTRACT LETTER OF REOUESTING/
AWARDED INTENT
NO.
2
2
2
5
5
1
1
2
1
1
2

-------
                                         TABLE  7
                                SUMMARY  OF  FGO  SYSTEMS BY  COMPANY
         UTILITY

TEXAS UTILITIES
TEXAS UTILITIES CO.
UNITED POWER ASSOCIATION
UTAH POWER « LIGHT  CO.
WISCONSIN POWER * LIGHT CO.
T fl T A 1
1 U 1 AL
OOPDATTOMAI
UrEKA j lUNAU


CONTRACT
AWAKUED
NO.
1
5
2
2
1
MU
750.
3922.
1090.
615.
527.
NO.
0
0
0
0
0
MU
0.
0.
0.
0.
0.
NO.
0
3
0
2
0
MW
0.
2336.
0.
615.
0.
NO.
0
2
2
0
0
MU
0.
1566.
1090.
0.
0.

LETTER OF REQUESTING/
INTENT
NO.
0
0
0
0
1
MW
0.
0.
o.
0.
527.
EVAL.
NO.
0
0
0
0
0
BIDS
MW
0.
0.
0.
0.
0.
CONSIDERING
FGO SYSTEMS
NO.
1
0
0
0
0
MW
750.
0.
0.
0.
o.
   TOTALS
119  50577.   27   7819.   29  126H8.   20   9797.
1692.
                                                                                                          3565.   33  14656.
                                                              206
                                                                                           PEDCo  ENVIRONMENTAL
                                                                                                 CINCINNATI. OHIO 45246

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           TABLE  S

SUMMARY OF FGD SYSTEMS BY VENDOR
                209
                                    PEDCo ENVIRONMENTAL
                                         CINCINNATI. OHIO 45246

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210
                        PEDCo  ENVIRONMENTAL
                             CINCINNATI. OHIO

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           TABLE  8
SUMMARY OF FGD SYSTEMS BY VENDOR

TOTAL OPERATIONAL CONSTRUCTION
MANUFACTURER/PROCESS
AOL/COMBUSTION EQUIP ASSOCIATE
LIME/ALKALINE FLYASH SCRUBBING
SODIUM CARBONATE SCRUBBING
TOTAL, ADL/COMBUSTION EQUIP ASS
AOL/COMBUSTION EQUIP. ASSOC.
LIME/ALKALINE FLYASH SCRUBBING
TOTAL, ADL/COMBUSTION EQUIP. AS
AMERICAN AIR FILTER
LIME SCRUBBING
TOTAL, AMERICAN AIR FILTER
BABCOCK X WILCOX
LIMESTONE SCRUBBING
TOTAL, BABCOCK ft UILCOX
BABCOCK AND WILCOX
LIME SCRUBBING
TOTAL, BABCOCK AND UILCOX
BUELL/ENVIROTECH
DOUBLE ALKALI SCRUBBING
TOTAL, BUELL/ENVIROTECH
CHEMICO
LIME SCRUBBING
LIME/LIMESTONE SCRUBBING
LIMESTONE SCRUBBING
TOTAL, CHEMICO
COMBUSTION ENGINEERING
LIME SCRUBBING
LIMESTONE SCRUBBING
TOTAL, COMBUSTION ENGINEERING
DAVY POWERGAS/ALLIEO CHEMICAL
WELLMAN LORD/ALLIED CHEMICAL
TOTAL. DAVY POWERGAS/ALLIED CHE
PEABODY ENGINEERING
LIMESTONE SCRUBBING
TOTAL, PEABODY ENGINEERING
NO.

2
3
5

1
1

4
4

4
4

2
2

1
1

6
1
1
8

4
6
10

3
3

1
1
MW

720.
375.
1095.

450.
450.

917.
917.

1451.
1451.

1250.
1250.

575.
575.

3405.
10.
750.
4165.

468.
3275.
3763.

830.
830.

225.
225.
NO.

2
3
5

0
0

2
2

2
2

0
0

0
0

3
1
0
4

3
4
7

1
1

0
0
MM

720.
375.
1095.

0.
0.

242.
242.

987.
987.

0.
0.

0.
0.

1755.
10.
0.
1765.

305.
1915.
2220.

115.
115.

0.
0.
NO.

0
0
0

1
1

2
2

2
2

2
2

1
1

3
0
1
4

1
2
3

2
2

1
1
MU

0.
0.
0.

450.
450.

675.
675.

464.
464.

1250.
1250.

575.
575.

1650.
0.
750.
2400.

183.
1360.
1543.

715.
715.

225,
225.
                                   211
                                                               PEDCo  ENVIRONMENTAL.
                                                                     CINCINNATI. OHIO -45246

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                                      TABLE S
                           SUMMARY  OF FGO SYSTEMS BY VENDOR
  MANUFACTURER/PROCESS
   TOTAL


NO.     MW
                                            	STATUS	

                                            OPERATIONAL  CONSTRUCTION
NO.
NO.
RESEARCH COTTRELL
 LIMESTONE SCRUBBING
TOTAL. RESEARCH COTTRELL

RILEY STOKER / ENVIRONEERING
 LIMESTONE SCRUBBING
TOTAL. RILEY STOKER / ENVIRONEE

RILEY STOKER/ENVIRONEERING
 LIMESTONE SCRUBBING
TOTAL. RILEY STOKER/ENVIRONEERI

TENNESSEE VALLEY AUTHORITY
 LIMESTONE SCRUBBING
TOTAL. TENNESSEE VALLEY AUTHORI

UNITED ENGINEERS / PECO
 MAGNESIUM OXIDE SCRUBBING
TOTAL. UNITED ENGINEERS / PECO

UNIVERSAL OIL PRODUCTS
 LIME SCRUBBING
 LIME/LIMESTONE SCRUBBING
 LIMESTONE SCRUBBING
TOTAL. UNIVERSAL OIL PRODUCTS
6
6
2
2
1
1
1
1
1
1
2
1
3
6
2351.
2351.
360.
3bO.
400.
«00.
550.
550.
120.
120.
800.
10.
1155.
1965.
1
1
0
0
0
0
1
1
1
1
1
1
1
3
115.
115.
0.
0.
0.
0.
550.
550.
120.
120.
400.
10.
200.
610.
5
5
2
2
1
1
0
0
0
0
1
0
2
3
2236.
2236.
360.
360.
400.
400.
0.
0.
0.
0.
400.
0.
955.
1355.
                                  56 20467.
                27  7fll9.
                29  1264B.
                                                               212
                                                                                            PEDCo  ENVIRONMENTAL

                                                                                                   CINCINNATI. OHIO 45246

-------
                    TABLE  9

SUMMARY OF NEW AND RETROFIT FGD SYSTEMS BY PROCESS
                         213
                                             PEDCo ENVIRONMENTAL
                                                  CINCINNATI. OHIO 45246

-------
PEDCo  ENVIRONMENTAL
     CINCINNATI. OHIO 45246

-------
                                                   TABLE 9
                                 SUMMARY OF NEW AND RETROFIT  FGO  SYSTEMS  BY  PROCESS
                                         MW CAPACITYCNO.  OF  PLANTS)
            PROCESS

LIME SCRUBBING
LIME/ALKALINE FLYASH
 (PROCESS NOT SELECTED)

LIME/ALKALINE FLYASH SCRUBBING
 (PROCESS NOT SELECTED)

LIME/LIMESTONE SCRUBBING
 (PROCESS NOT SELECTED)

LIMESTONE SCRUBBING
  SUBTOTAL - LIME/LIMESTONE
 AQUEOUS  CARBONATE SCRUBBING
 DOUBLE  ALKALI  SCRUBBING
 MAGNESIUM  OXIDE  SCRUBBING
 NOT SELECTED
 REGENERABLE  NOT  SELECTED
 SODIUM CARBONATE  SCRUBBING
 WELLMAN LORD/ALLIED  CHEMICAL
           TOTALS
  LIME/LIMESTONE * OF  TOTAL MW
NEW OR OPERATIONAL
RETROFIT

N
R
N
R
; N
R
N
R
N
R
N
R
N
R
N
R
N
R
N
R
N
R
N
R
N
R
N
R
U N
R
NO.
2
7
0
0
2
0
0
2
5
4
9.
13.
0
0
0
0
0
1
0
0
0
0
1
2
0
1
10.
17.


MW
1235
1467
0
0
720
0
0
20
2610
957
4765.
2444.
0
0
0
0
0
120
0
0
0
0
125
250
0
115
4890.
2929.
97
63
CONSTRUCTION
NO. MW
8
1
0
0
1
0
0
0
15
1
24
2
0
0
1
0
0
0
0
0
0
0
0
0
1
1
26
3


3975
103
0
0
450
0
0
0
6325
425
.10750.
. 608.
0
0
575
0
0
0
0
0
0
0
0
0
375
340
.11700.
. 948.
92
64
CONTRACT
AWARDED
NO.
4
0
0
0
2
0
0
0
10
0
16.
0.
0
1
1
1
0
0
0
0
0
0
1
0
0
0
18.
2.


MW
235o
0
0
0
1400
0
0
0
4911
0
8661.
0.
0
100
230
277
0
0
0
0
0
0
509
0
0
0
9420.
377.
92
0
LETTER OF RE8UESTING/
INTENT EVAL. BIOS
NO.
0
0
1
0
1
0
0
0
0
0
2.
0.
0
0
0
0
0
1
0
0
1
0
1
0
0
0
4.
1.


MW
0
0
527
0
500
0
0
0
0
0
1027.
0.
0
0
0
0
0
240
0
0
500
0
125
0
0
0
1652.
240.
62
0
NO.
0
0
0
0
0
0
0
0
1
0
1.
o.
0
0
0
0
0
0
4
0
0
0
0
0
0
0
5.
0.


MW
0
0
0
0
0
0
0
0
545
0
545.
0.
0
0
0
0
0
0
3020
0
0
0
0
0
0
0
3565.
0.
15
0
CONSIDERING
FGO SYSTEM
NO.
0
2
0
0
1
0
0
0
3
1
4.
3.
0
0
0
0
0
2
16
6
1
1
0
0
0
0
21.
12.


MW
0
66Q
0
0
450
0
0
0
1280
350
1730.
1010.
0
0
0
0
0
486
8000
2480
500
650
0
0
0
0
10230.
4626.
17
22
TOTAL NO.
OF PLANTS
NO.
14
10
1
0
7
0
0
2
34
6
56.
18.
0
1
2
1
0
4
20
6
2
1
3
2
1
2
84.
35.


MW
7560
2310
527
0
3520
0
0
20
15871
1732
27478.
4062.
0
100
825
277
0
846
11020
2480
1000
650
759
250
375
455
41457.
9120.
66
45
                                                               215
                                                                                          PEDCo  ENVIRONMENTAL
                                                                                                 CINCINNATI. OHIO 45246

-------
216
                       PEDCo  ENVIRONMENTAL
                            CINCINNATI. OHIO

-------
                           TABLE 10

SUMMARY OF OPERATING FGD SYSTEMS BY PROCESS AND GENERATING UNITS
                                217
                                                    PEDCo ENVIRONMENTAL
                                                         CINCINNATI. OHIO 45246

-------
216
                       PEDCo ENVIRONMENTAL
                             CINCINNATI. OHIO

-------
                      TABLE  10
           SUMMARY  OF  OPERATING  FGD  SYSTEMS  BY
           PROCESS  AND GENERATING  UNITS  AS Of 06/77
  PROCESS/GENERATING  UNITS
FGD/MW  STARTUP  EXPERIENCE(MO.)
LIME SCRUBBING
BRUCE MANSFIELD NO. 1
CANE RUN NO 4
CONESVILLE NO 5
ELRAMA POWER STATION
GREEN RIVER NOS. 1 2 AND 3
HAWTHORN NO. 3
HAWTHORN NO. 4
PADDYS RUN NO 6
PHILLIPS POWER STATION

LIME/ALKALINE FLYASH
COLSTRIP NO 1
COLSTRIP NO 2

835
178
400
510
64
140
100
6S
410
2702.
SCRUBBING
360
360

4-76
8-76
2-77
10-75
9-75
11-72
8-72
4-73
7-73


10-75
7-76

14
10
i*
20
21
55
58
50
47
279

20
11
                                    720.
                                                               31
        LIME/LIMESTONE SCRUBBING
SHAUNEE N0.10A
SHAwNEE N0.10B
    10
    10
                                     20.
 1-72
 4-72
 62
 62

124
        LIMESTONE SCRUBBING
CHOLLA NO 1
LA CY6NE NO 1
LAURENCE NO 4
LAURENCE NO 5
SHERBURNE COUNTY STATION NO.I
SHERBURNE COUNTY STATION NO.2
SOUTHWEST NO. 1
WIDOWS CREEK NO. 8
WILL COUNTY NO 1
   115
   82U
   400
   710
   680
   20U
   b50
   167
10-73
 2-73
12-68
 6-76
 3-76
 4-77
 4-77
 5-77
 2-72
                                   3767.
 44
 52
102
-12
 15
  2
  2
  1
 64

270
                                                            219
                                                                                        PEDCo  ENVIRONMENTAL
                                                                                               CINCINNATI. OHIO 45246

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                      TABLE 10
           SUMMARY OF OPERATING FGO SYSTEMS BY
           PROCESS AND GENERATING UNITS AS OF 06/77
  PROCESS/GENERATING UNITS         FGO/MU  STARTUP  EXPERIENCE(MO.)



        MAGNESIUM OXIDE SCRUBBING

EDDYSTONE NO. 1A                     120     9-75              21

                                    120.                       21


        SODIUM CARBONATE SCRUBBING

REID GARDNER NO 1                    125     H-7H              36
REID GARDNER NO 2                    125     H-7H              36
REID GARDNER NO 3                    125     7-76              11

                                    375.                       87


        UELLHAN LORD/ALLIED CHEMICAL

D.H. MITCHELL NO.11                  115     6-77               0
D.H. MITCHELL NO.11                  3HO    11-77              -5

                                    155.                       -5
                                                            220
                                                                                        PEDCo  ENVIRONMENTAL
                                                                                               CINCINNATI. OHIO  45246

-------
                           TABLE 11

SUMMARY OF SLUDGE DISPOSAL PRACTICES FOR OPERATIONAL FGD SYSTEMS
                                221
                                                   PEDCo  ENVIRONMENTAL
                                                         CINCINNATI. OHIO 45246

-------
222
                         PEDCo  ENVIRONMENTAL
                               CINCINNATI. OHIO 452.46

-------
                            TABLE  11
        SUMMARY OF SLUDGE DISPOSAL PRACTICES  FOR OPERATIONAL FGO SYSTEMS AS OF  06/77
PROCESS/GENERATING UNIT
—SLUDGE—      --SLUDGE--       ---POND	      	POND--
STABILI2EO    UNSTABILIZED        LINED          UNLINED
      LIME SCRUBBING

BRUCE MANSFIELD NO. 1
CANE RUN NO 4
CONESVILLE NO 5
ELRAMA POWER STATION
GREEN RIVER NOS. 1  2  AND 3
HAWTHORN NO. 3
HAWTHORN NO. 4
PADDYS RUN NO 6
PHILLIPS POWER STATION

      TOTAL
       635
       178
       too
       510
        64
       410

      2397.
                       140
                       100
                        65
 305.
                635
                178
                400
                510
                 64
                140
                100
                 65
                410

                2702.
      LIME/ALKALINE FLYASH SCRUBBING
 COLSTRIP NO 1
 COLSTRIP NO 2

       TOTAL
          0.
 360
 360

 720.
                 360
                 360

                 720,
       LIMESTONE  SCRUBBING

 CHOLLA NO 1
 LA CTGNE NO  1
 LAWRENCE NO  4
 LAWRENCE NO  5
 SHERBURNE COUNTY STATION NO.l
 SHERBURNE COUNTY STATION NO.2
 SOUTHWEST NO.  1
 WIDOWS CREEK NO. 8
 WILL COUNTY  NO 1

       TOTAL
        200

        167

        367.
 115
 620
 125
 400
 710
 680

 550
3400.
                                       710
                                       660
 167

1557.
                                                       115
                                                       620
                                                       125
                                                       400
                 200
                 550
                                                                                          2210.
       SODIUM CARBONATE  SCRUBBING
 REID GARDNER  NO  1
 REID GARDNER  NO  2
 REID GARDNER  NO  3

       TOTAL
                                             0.
                       125
                       125
                       125

                       375.
                   0.
                                                        223
                 125
                 125
                 125

                 375.
                                                  PEDCo  ENVIRONMENTAL-
                                                         CINCINNATI. OHIO 452.46

-------
                            TABLE:  11
        SUMMARY  OF  SLUDGE  DISPOSAL  PRACTICES  FOR  OPERATIONAL FGD  SYSTEMS  AS  OF   06/77
PROCESS/GENERATING  UNIT
--SLUDGE--
STABILIZED
  --SLUDGE--
UNSTABILIZED
	POND-
  LINED
                                                                                    	POND--
                                                                                    UNLINED
                                                                                      PEDCo  ENVIRONMENTAL
                                                                                            CINCINNATI. OHIO 45246

-------
                      TABLE 12

SUMMARY OF FGD SYSTEMS BY PROCESS AND REGULATORY CLASS
                           225
                                               PEDCo ENVIRONMENTAL
                                                    CINCINNATI. OHIO 45246

-------
PEDCo  ENVIRONMENTAL
     CINCINNATI. OHIO 45246

-------
                                                   TABLE 12
                                 SUMMARY OF FGO SYSTEMS BY  PROCESS AND REGULATORY  CLASS

                                         MU CAPACITYINO. OF PLANTS)
            PROCESS

LIME SCRUBBING
LIME/ALKALINE FLYASH
 (PROCESS NOT SELECTED)
CLASS

   A
   B
   C
   D
   E

   A
   B
   C
   0
   E
LIME/ALKALINE FLYASH SCRUBBING
  (PROCESS NOT SELECTED)
 LIME/LIMESTONE  SCRUBBING
  I PROCESS NOT SELECTED)
 LIMESTONE SCRUBBING
   SUBTOTAL - LIME/LIMESTONE
   A
   B
   C
   D
   E

   A
   B
   C
   D
   E

    A
    B
    C
    0
    E
    A
    B
    C
    D
    "E
OPERATIONAL
CONSTRUCTION
CONTRACT
AWARDED
NO.
0
6
3
0
0
0
0
0
0
0
0
2
0
0
0
0
0
2
0
0
1
3
3
2
0
1.
11.
8.
2.
0.
nw
0
2395
307
0
0
0
0
0
0
0
0
720
0
0
0
0
0
20
0
0
200
1505
1537
525
0
200.
4620.
1864.
525.
0.
NO.
6
2
1
0
0
0
0
0
0
0
0
1
0
0
0
0
0
0
0
0
10
5
1
0
0
16.
a.
2.
0.
0.
nw
27*0
1235
163
0
0
0
0
0
0
0
0
450
0
0
0
0
0
0
0
0
1*315
2010
425
0
0
7055.
3695.
606.
0.
0.
NO.
3
1
0
0
0
0
0
0
0
0
0
2
0
0
0
0
0
0
0
0
3
6
0
0
1
6.
9.
0.
0.
1.
nw
1515
835
0
0
0
0
0
0
0
0
0
moo
0
0
0
0
0
0
0
0
1811
2700
0
0
400
3326.
«t935.
0.
0.
400.
LETTER OF REQUESTING/
INTENT
NO.
0
0
0
0
0
1
0
0
0
u
1
0
0
0
0
0
0
0
0
0
0
0
0
0
0
2.
0.
0.
o.
0.
nw
0
0
0
0
0
527
0
0
0
0
500
0
0
0
0
0
0
0
0
0
0
0
0
0
0
1027.
0.
0.
0.
o.
EVAL.
NO.
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
1
0
0
0
0
1.
0.
0.
0.
0.
BIDS
MW
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
5*5
0
0
0
0
5i*5.
0.
0.
0.
0.
CONSIDERING
TUTAU NU.
OF PLANTS
FGD SYSTEM
NO.
0
0
2
0
0
0
0
0
0
0
0
1
0
0
0
0
0
0
0
0
2
1
0
0
1
2.
2.
2.
0.
1.
nw
0
0
660
0
0
0
0
0
0
0
0
450
0
0
0
0
0
0
0
0
930
350
0
0
350
930.
800.
660.
0.
350.
NO.
9
9
6
0
0
1
0
0
0
0
1
6
0
0
0
0
0
2
0
0
17
15

-------
                                                   TABLE 12
                                 SUMMARY  OF  FGD SYSTEMS BY PROCESS AND REGULATORY CLASS

                                         MW  CAPACITYJNO. OF PLANTS*
                            REGULATORY OPERATIONAL  CONSTRUCTION
            PROCESS

AQUEOUS CARBONATE SCRUBBING
DOUBLE ALKALI SCRUBBING
MAGNESIUM OXIOE SCRUBBING
NOT SELECTED
REGENERAeLE NOT SELECTED
CLA^SS

   A
   B
   C
   D
   e

   A
   B
   C
   D
   E

   A
   B
   C
   D
   E

   A
   B
   C
   0
   E

   A
   B
   C
   D
   E
NO.
 0
 0
 0
 0
 0

 0
 0
 0
 u
 0

 0
 1
 0
 0
 u

 0
 0
 0
 u
 0

 0
 0
 0
 0
 0
  MW
  0
  0
  0
  0
  0

  0
  0
  0
  0
  0

  0
120
  0
  0
  0

  0
  0
  0
  0
  0

  0
  0
  0
  0
  0
NO.
 0
 0
 0
 0
 0
MW
0
0
0
0
0
 I   575
 0     0
 0     0
 0     0
 0     0
       0
       0
       0
       0
       0

       0
       0
       0
       0
       0

       0
       0
       0
       0
       0
CONTRACT
AWARDED
NO.
0
0
1
0
0
1
0
1
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
MW
0
0
100
0
0
250
0
277
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
LETTER OF REOUESTING/
INTENT
NO.
0
0
0
0
0
0
0
0
0
0
0
1
0
0
0
0
0
0
0
0
0
1
0
0
0
MW
0
0
0
0
0
0
0
0
0
0
0
2tO
0
0
0
0
0
0
0
0
0
500
0
0
0
EVAL
NO.
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
n
0
0
0
0
0
0
0
0
0
. BIDS
MW
0
0
0
0
0
0
0
0
0
0
0
0
0
0
0
3020
0
0
0
0
0
0
0
0
0
CONSIDERING
TU1AL NU.
OF PLANTS
FGD SYSTEM
NO.
0
0
0
0
0
0
0
0
0
0
0
2
0
0
0
4
13
<4
0
1
0
1
1
0
0
MW
0
0
0
0
0
0
0
0
0
0
0
486
0
0
0
2600
6160
970
0
750
0
500
65Q
0
0
NO.
0
0
1
0
0
2
0
1
0
0
0
4
0
0
0
8
13
H
0
1
0
2
1
0
0
MW
0
0
100
0
0
825
0
277
0
0
0
8<»6
0
0
0
5620
6160
970
0
750
0
1000
65o
0
0
  A.  BOILER CONSTRUCTED SUBJECT TO FEDERAL NSPS
  B.  BOILER SUBJECT TQ STATE STANDARD THAT IS MORE STRINGENT THAN THE FEDERAL NSPS
  C.  BOILER SUBJECT To STATE STANDARD THAT IS EQUAL TO OR LLSS STRINGENT THAN NSPS
  D.  OTHER
  E.  REGULATORY CLASS UNKNOWN
                                                               226
                                                                                            PEDCo  ENVIRONMENTAL
                                                                                                  CINCINNATI. OHIO 45246

-------
                                                   TABLE. 12
                                 SUMMARY OF FGD SYSTEMS BY PROCESS AND REGULATORY CLASS

                                         Mw CAPACITY(NO. OF PLANTS)
            PROCESS

SODIUM CARBONATE SCRUBBING
WELLMAN LORD/ALLIED CHEMICAL
          TOTALS
   LIME/STONE  X  OF  TOTAL MW
CLASS

   A
   B
   C
   D
   E

   A
   B
   C
   0
   E
    A
    B
    C
    D
    E

    A
    B
    C
    0
    E
f OPERATIONAL
CONSTRUCTION
CONTRACT
AWARDED
NO. MW
0
3
0
0
U
0
0
1
0
0
1
15
9
2
0





0
375
0
0
0
0
0
115
0
0
200.
. 5115.
. 1979.
525.
0.
100
90
9t
100
0
NO. MW
0
0
0
0
0
0
2
0
0
0
17
10
2
0
0





0
0
0
0
0
0
715
0
0
0
. 7630.
. HtlO.
. 606.
0.
0.
92
81
100
0
0
NO.
0
1
0
0
0
0
0
0
0
0
7.
10.
2.
0.
1.





MW
0
509
0
0
0
0
0
0
0
0
3576.
5 •»•»<».
377.
0.
too.
93
91
0
0
100
LETTER OF REQUESTING/
INTENT
NO.
0
1
0
0
0
0
0
0
0
0
2.
3.
0.
o.
o.





MW
0
125
0
0
0
0
0
0
0
0
1027.
865.
0.
0.
0.
100
0
0
0
0
EVAL.
NO.
0
0
0
0
0
0
0
0
0
0
5.
0.
0.
0.
0.





BIOS
MW
0
0
0
0
0
0
0
0
0
0
3565.
0.
0.
0.
0.
15
0
0
0
0
CONSIDERING
TOTAL NO.
OF PLANTS
FGD SYSTEM
NO.
0
0
0
0
0
0
0
0
0
0
6.
16.
7.
0.
2.





MW
0
0
0
0
0
0
0
0
0
0
3530.
79«*6.
2260.
0.
1100.
26
10
29
0
32
NO.
0
5
0
0
0
0
2
1
0
0
36.
56.
20.
2.
3.





MW
0
1009
0
0
0
0
715
115
0
0
19526,
23780.
52<»<».
525.
1500.
67
59
60
100
50
   A.  BOILER CONSTRUCTED SUBJECT TO FEDERAL NSPS
   B.  BOILER SUBJECT To STATE STANDARD THAT IS MORE  STRINGENT  THAN  THE  FEDERAL  NSPS
   C.  BOILER SUBJECT TO STATE STANDARD THAT IS EiUAL TO  OR  LLSS  STRINGENT  THAN  NSPS
   D.  OTHER
   E,  REGULATORY CLASS UNKNOWN
                                                                229
                                                                                           PEDCo  ENVIRONMENTAL
                                                                                                  CINCINNATI. OHIO 45246

-------
230
                        PEDCo  ENVIRONMENTAL
                              CINCINNATI. OHIO 45246

-------
            TABLE 13

SUMMARY OF OPERATIONAL FGD SYSTEMS
                 231
                                     PEDCo ENVIRONMENTAL
                                          CINCINNATI. OHIO 45246

-------
232
                      PEDCo ENVIRONMENTAL
                            CINCINNATI. OHIO

-------
                      TABLE 13
            SUMMARY OF OPERATIONAL FGD SYSTEMS AS OF 06/77
       UTILITY COMPANY
        POWER STATION
 NEW OR   SIZE. OF FGD  PROCESS/VENDOR
RETROFIT   UNIT (nui
 FUEL CHARACTERISTICS
MO/YR
ARIZONA PUBLIC SERVICE
CHOLLA NO 1


COLUMBUS ft SOUTHERN OHIO ELEC.
CONESVILLE NO 5

COMMONWEALTH EDISON
WILL COUNTY NO I

OUQUESNE LIGHT
ELRAMA POWER STATION

DUQUESNE LIGHT
PHILLIPS POWER STATION

KANSAS CITY  POWER  ft LIGHT
HAWTHORN NO.  4

KANSAS  CITY  POWER  X LIGHT
LA CYGNE NO  1

KANSAS CITY  POWER  ft LIGHT
HAWTHORN NO. 3

KANSAS POWER ft  LIGHT
 LAWRENCE NO  0

 KANSAS POWER ft LIGHT
 LAWRENCE NO 3

 KENTUCKY UTILITIES
 GREEN RIVER NOS. 1  2  AND 3

 LOUISVILLE GAS ft ELECTRIC
 CANE RUN NO 4

 LOUISVILLE GAS ft ELECTRIC
 PADDYS RUN NO 6

 MONTANA POWER CO.
 COLSTRIP NO 1


 MONTANA POWER CO.
 COLSTRIP NO 2
R
N
R
R
R
R
N
R
R
N
R
R
R
N
N
115
400
167
510
410
100
820
110
125
400
64
176
65
360
360
                      RESEARCH COTTRELL
                      LIMESTONE SCRUBBING

                      UNIVERSAL OIL PRODUCTS
                      LIME SCRUBBING

                      BABCOCK ft WILCOX
                      LIMESTONE SCRUBBING

                      CHEMICO
                      LIME SCRUBBING

                      CHEMICO
                      LIME SCRUBBING

                      COMBUSTION  ENGINEERING
                      LIME SCRUBBING

                      BABCOCK  ft WILCOX
                      LIMESTONE SCRUBBING

                      COMBUSTION  ENGINEERING
                      LIME SCRUBBING

                      COMBUSTION  ENGINEERING
                      LIMESTONE  SCRUBBING

                      COMBUSTION  ENGINEERING
                      LIMESTONE  SCRUBBING

                      AMERICAN AIR FILTER
                      LIME  SCRUBBING

                      AMERICAN AIR FILTER
                      LIME  SCRUBBING

                      COMBUSTION  ENGINEERING
                      LIME  SCRUBBING

                      ADL/COMBUSTION  EQUIP ASSOCIATE
                      LIME/ALKALINE FLYASH SCRUBBING

                      ADL/COMBUSTION  EQUIP ASSOCIATE
                      LIME/ALKALINE FLYASH SCRUBBING
COAL   0.44-1 PERCENT SULFUR    10/73
COAL  4.5 - 4.9 PERCENT SULFUR   2/77
COAL 4.0 PERCENT SULFUR          2/72
COAL  i.o - 2.8 PERCENT SULFUR  10/75
COAL   i.o- 2.8 PERCENT SULFUR   7/73
COAL   0.5-3.5 PERCENT SULFUR    8/72
COAL  5.0 PERCENT SULFUR          2/73
 COAL    0.5-3*5  PERCENT SULFUR   11/72
 COAL  0.5  PERCENT  SULFUR         12/68
 COAL 0.5 PERCENT  SULFUR          6/78
 COAL  3.8 PERCENT  SULFUR         9/75
 COAL 3.5 -  4.0  PERCENT  SULFUR     8/76
 COAL 3.5 -  4.0  PERCENT  SULFUR    4/73
 COAL  0.8  PERCENT  SULFUR          10/75
 COAL  0.8  PERCENT  SULFUR          7/76
                                                               233
                                                                                          PEDCo  ENVIRONMENTAL
                                                                                                 CINCINNATI. OHIO 45246

-------
                      TABLE 13
            SUMMARY OF OPERATIONAL F6D SYSTEMS AS OF 06/77
       UTILITY COMPANY
        POWER STATION
 NEW OR   SIZE OF FGD  PROCESS/VENDOR
RETROFIT   UNIT 
                                 FUEL CHARACTERISTICS
                                MO/YR
NEVADA POWER
REID GARDNER NO 2
NEVADA POWER
REID GARDNER NO 1
NEVADA POWER
REID GARDNER NO 3
NORTHERN INDIANA PUB SERVICE
O.H. MITCHELL NO.11
NORTHERN STATES POWER CO.
SHERBURNE COUNTY STATION NO.l
NORTHERN STATES POWER co.
SHERBURNE COUNTT STATION NO.2
PENNSYLVANIA POWER CO.
BRUCE MANSFIELD NO. 1
PHILADELPHIA ELECTRIC CO.
EDOYSTONE NO. 1A
SPRINGFIELD CITY UTILITIES
SOUTHWEST NO. 1
TENNESSEE VALLEY AUTHORITY
SHAWNEE N0.10A
TENNESSEE VALLEY AUTHORITY
SHAWNEE N0.10B
TENNESSEE VALLEY AUTHORITY
WIDOWS CREEK NO. 6
R
R
N
R
N
N
N
R
N
R
R
R
125
125
125
115
710
680
835
120
200
10
10
550
AOL/COMBUSTION EQUIP ASSOCIATE
SODIUM CARBONATE SCRUBBING
AOL/COMBUSTION EQUIP ASSOCIATE
SODIUM CARBONATE SCRUBBING
AOL/COMBUSTION EQUIP ASSOCIATE
SODIUM CARBONATE SCRUBBING
DAVY POWERGAS/ALLIED CHEMICAL
WELLMAN LORD/ALLIED CHEMICAL
COMBUSTION ENGINEERING
LIMESTONE SCRUBBING
COMBUSTION ENGINEERING
LIMESTONE SCRUBBING
CHEMICO
LIME SCRUBBING
UNITED ENGINEERS / PECO
MAGNESIUM OXIDE SCRUBBING
UNIVERSAL OIL PRODUCTS
LIMESTONE SCRUBBING
UNIVERSAL OIL PRODUCTS
LIME/LIMESTONE SCRUBBING
CHEMICO
LIME/LIMESTONE SCRUBBING
TENNESSEE VALLEY AUTHORITY
LIMESTONE SCRUBBING
COAL 0.5 - 1.0 PERCENT SULFUR    "»/7<»
COAL 0.5 • 1.0 PERCENT SULFUR    H/7H
COAL 0.5 - 1.0 PERCENT SULFUR    7/76
COAL 3.2-3.5 PERCENT SULFUR      6/77
COAL 0.8 PERCENT SULFUR          3/76
COAL 0.8 PERCENT SULFUR          H/77
COAL 4.7 PERCENT SULFUR          
-------
                TABLE m

SUMMARY OF F6D SYSTEMS UNDER CONSTRUCTION
                     235
                                         PEDCo ENVIRONMENTAL
                                              CINCINNATI. OHIO 49246

-------
236
                        PEDCo  ENVIRONMENTAL
                             CINCINNATI. OHIO 45246

-------
                      TABLE 1*
            SUMMARY OF FGD SYSTEMS UNDEK CONSTRUCTION AS OF 06/77
       UTILITY COMPANY
        POWER STATION
 NEW OR   SIZE OF FGO  PROCESS/VENDOR
RETROFIT   UNIT IMWI
 FUEL CHARACTERISTICS
                                                                                                                      HO/YR
ALABAMA ELECTRIC COOP
TOMBIGBEE NO. 2

ALLEGHENY POWER SYSTEM
PLEASANTS NO. 2

ALLEGHENY POWER SYSTEM
PLEASANTS NO. 1

ARIZONA ELECTRIC POWER COOP
APACHE NO 2

ARIZONA ELECTRIC POWER COOP
APACHE NO 5

ARIZONA PUBLIC  SERVICE
CHOLLA NO 2

BIG RIVERS ELECTRIC COOP CORP.
REID NO.  2

CENTRAL  ILLINOIS LIGHT  CO.
DUCK CREEK NO.  1

CENTRAL ILLINOIS PUBLIC SERV
NEWTON NO.l

 COLUMBUS ft SOUTHERN OHIO ELEC.
 CONESVILLE NO 6

 COMMONWEALTH EDISON
 POWERTON NO. 51

 INDIANAPOLIS POWER ft LIGHT CO.
 PETERSBURG NO 3

 KANSAS POWER S LIGHT
 JEFFERY NO.  1

 KANSAS POWER * LIGHT
 JEFFERY NO.  2

 LOUISVILLE GAS & ELECTRIC
 CANE RUN NO 5
N
N
N
N
N
N
N
N
N
N
R
N
N
N
R
225
625
625
200
200
250
250
000
575
*00
025
530
680
680
183
                      PEABODY ENGINEERING
                      LIMESTONE SCRUBBING

                      BABCOCK AND WILCOX
                      LIME SCRUBBING

                      BABCOCK AND WILCOX
                      LIME SCRUBBING

                      RESEARCH COTTRELL
                      LIMESTONE SCRUBBING

                      RESEARCH COTTRELL
                      LIMESTONE SCRUBBING

                      RESEARCH COTTRELL
                      LIMESTONE SCRUBBING

                      AMERICAN AIR  FILTER
                      LIME  SCRUBBING

                      RILEY STOKER/ENVIRONEERING
                      LIMESTONE  SCRUBBING

                      BUELL/ENVIROTECH
                      DOUBLE ALKALI SCRUBBING

                      UNIVERSAL  OIL PRODUCTS
                      LIME  SCRUBBING

                      UNIVERSAL  OIL PRODUCTS
                      LIMESTONE  SCRUBBING

                      UNIVERSAL  OIL PRODUCTS
                      LIMESTONE  SCRUBBING

                      COMBUSTION ENGINEERING
                      LIMESTONE  SCRUBBING

                      COMBUSTION ENGINEERING
                      LIMESTONE  SCRUBBING

                      COMBUSTION ENGINEERING
                      LIME  SCRUBBING
COAL   0.6- 1.5 PERCENT SULFUR   6/78
COAL 4.5 PERCENT SULFUR (MAXI    3/80
COAL 1.5 PERCENT SULFUR (MAX)    3/79
COAL  0.5- 0.8 PERCENT SULFUR    6/78
COAL   o.s- 0.8 PERCENT SULFUR   1/79
COAL   0.10-1 PERCENT SULFUR
 6/78
COAL  3.S-H.O PERCENT SULFUR     12/79


COAL  2.5  -  3.0 PERCENT SULFUR    8/78


COAL  2.8-3.2 PERCENT SULFUR     11/79


COAL   i».5 - *.9  PERCENT  SULFUR   1/78
 COAL 3.6 PERCENT  SULFUR
12/79
 COAL  3.0-3.5  PERCENT  SULFUR      9/77
 COAL 0.30  PERCENT  SULFUR
 COAL 0.30  PERCENT  SULFUR
 6/78
 6/79
 COAL 3.5 -  H.O  PERCENT  SULFUR    12/77
                                                               237
                                                                                           PEDCo  ENVIRONMENTAL
                                                                                                  CINCINNATI. OHIO 45246

-------
                      TABLE l«t
            SUMMARY OF FGO SYSTEMS UNDER CONSTRUCTION AS OF 06/77
       UTILITY COMPANY
        POWER STATION
 NEW OR   SIZE OF FGO  PROCESS/VENDOR
RETROFIT   UNIT 
                                          FUEL CHARACTERISTICS
                                MO/YR
LOUISVILLE GAS t ELECTRIC
HILL CREEK NO 3

MINNKOTA POWER COOPERATIVE
HILTON R. YOUNG NO. 2

PENNSYLVANIA POWER CO.
BRUCE MANSFIELD NO. 2

PUBLIC SERVICE CO OF NEW MEX.
SAN JUAN NO. i

PUBLIC SERVICE CO OF NEW MEX.
SAN JUAN NO. 2

SOUTH CAROLINA PUBLIC SERVICE
WINYAH NO. 2

SOUTHERN ILLINOIS POWER CO OP
MARION NO. H

SOUTHERN MISSISSIPPI ELECTRIC
R.D. MORROW NO.l

SOUTHERN MISSISSIPPI ELECTRIC
R.O. MORROW NO.2

TEXAS UTILITIES CO.
MONTICELLO NO.3

TEXAS UTILITIES CO.
MARTIN LAKE NO. i

TEXAS UTILITIES co.
MARTIN LAKE NO. 2

UTAH POWER I LIGHT CO.
HUNTING!ON NO.l

UTAH POWER X LIGHT CO.
EMERY NO.l
N
N
R
N
N
N
N
N
N
N
635
375
3«»0
260
16*
160
160
750
793
793
«»25      AMERICAN AIR FILTER
         LIME SCRUBBING

450      AOL/COMBUSTION EQUIP. ASSOC.
         LIME/ALKALINE FLYASH SCRUBBING
         CHEMICO
         LIME SCRUBBING

         DAVY POWERGAS/ALLIED CHEMICAL
         WELLMAN LORD/ALLIED CHEMICAL

         DAVY POWERGAS/ALLIED CHEMICAL
         WELLMAN LORD/ALLIED CHEMICAL

         BABCOCK ft WILCOX
         LIMESTONE SCRUBBING

         BABCOCK ft WILCOX
         LIMESTONE SCRUBBING

         RILEY STOKER / ENVIRONEERING
         LIMESTONE SCRUBBING

         RILEY STOKER / ENVIRONEERING
         LIMESTONE SCRUBBING

         CHEMICO
         LIMESTONE SCRUBBING

         RESEARCH COTTRELL
         LIMESTONE SCRUBBING

         RESEARCH COTTRELL
         LIMESTONE SCRUBBING

         CHEMICO
         LIME SCRUBBING
«00      CHEMICO
         LIME SCRUBBING
COAL   3.5- <».o PERCENT SULFUR  12/77
LIGNITE - 6.500 BTU, 0.7* S      6/77
COAL H,7 PERCENT SULFUR         10/77
COAL   0.6 PERCENT SULFUR       11/77
COAL   0.8 PERCENT SULFUR       11/77
COAL  1.0 PERCENT SULFUR         7/77
COAL   4.5-5.0 PERCENT SULFUR    6/76
COAL 1.0 PERCENT SULFUR         11/77
COAL 1.0 PERCENT SULFUR          8/78
LIGNITE i.o PERCENT SULFUR       2/78
COAL   1.0 PERCENT SULFUR       10/77
COAL   1.0 PERCENT SULFUR        2/78
COAL  0.5 PERCENT SULFUR        12/77
COAL 0.5 PERCENT SULFUR          6/76
                                                              238
    PEDCo  ENVIRONMENTAL
           CINCINNATI, OHIO -45246

-------
          TABLE 15



SUMMARY OF PLANNED FGD SYSTEMS
               239
                                  PEDCo  ENVIRONMENTAL
                                        CINCINNATI. OHIO

-------
2 "40
                        PEDCo ENVIRONMENTAL
                              CINCINNATI. OHIO

-------
                   TABLE 15
            SUMMARY or PLANNED FGD SYSTEMS AS OF 06/77
       UTILITY COMPANY
        POWER STATION
 NEW OR   SIZE OF FGD  VENDOR/PROCESS
RETROFIT   UNIT CMWI
 FUEL CHARACTERISTICS
MO/YR
            CONTRACTS AWARDED

COLORADO UTE ELECTRIC ASSN.
CRAIG NO. 2
COLORADO UTE ELECTRIC ASSN.
CRAIG NO. 1

BRAZOS ELECTRIC POWER COOP
ATACOSA MCMULLEN NO. i

LOUISVILLE GAS ft ELECTRIC
CANE RUN NO 6

PACIFIC POWER AND LIGHT  CO.
JIM BRIDGER NO. 4

MONTANA POWER CO.
COLSTRIP NO. 3

MONTANA  POWER CO.
COLSTRIP NO. 4

BASIN ELECTRIC  POWER COOP
LARAMIE  RIVER NO.  2

 PENNSYLVANIA POWER CO.
 BRUCE MANSFIELD NO. 3

 LOUISVILLE GAS  * ELECTRIC
 MILL CREEK NO 4

 BASIN ELECTRIC  POWER COOP
 LARAMIE RIVER NO.  1
 NIAGARA MOHAWK  POWER COOP.
 CHARLES R. HUNTLEY NO.6

 ALABAMA ELECTRIC COOP
 TOMBI6BEE NO.  3

 TEXAS UTILITIES CO.
 MARTIN LAKE NO. 3

UNITED POWER ASSOCIATION
COAL  CREEK NO.  2
N
N
N
R
N
N
N
N
N
N
N
R
N
N
N
450
450
400
277
509
700
700
550
ess
425
550
100
225
793
545
                      PEABODY ENGINEERING
                      LIMESTONE SCRUBBING

                      PEABODY ENGINEERING
                      LIMESTONE SCRUBBING

                      BABCOCK ft WILCOX
                      LIMESTONE SCRUBBING

                      AOL/COMBUSTION EQUIP ASSOCIATE
                      DOUBLE ALKALI SCRUBBING

                      UNIVERSAL OIL PRODUCTS
                      SODIUM CARBONATL SCRUBBING

                      ADL/COMBUSTION EQUIP ASSOCIATE
                      LIME/ALKALINE FLYASH SCRUBBING

                      ADL/COMBUSTION EQUIP ASSOCIATE
                      LIME/ALKALINE FLYASH SCRUBBING

                      RESEARCH COTTRELL
                      LIMESTONE SCRUBBING

                      PULLMAN  KELLOGG
                      LIME SCRUBBING

                      AMERICAN AIR FILTER
                      LIME SCRUBBING

                      RESEARCH COTTRELL
                      LIMESTONE SCRUBBING

                      ATOMICS  INTERNATIONAL
                      AQUEOUS  CARBONATE  SCRUBBING

                      PEABODY  ENGINEERING
                      LIMESTONE SCRUBBING

                      RESEARCH COTTRELL
                      LIMESTONE SCRUBBING

                      COMBUSTION  ENGINEERING
                      LIME SCRUBBING
COAL 0.45 PERCENT SULFUR         3/79
COAL 0.45 PERCENT SULFUR         3/79
LIGNITE 1.67 PERCENT SULFUR     12/79
COAL 3.5 - 4.0 PERCENT SULFUR    2/79
COAL 0.56 PERCENT SULFUR(AVG.)   9/79
COAL  0.7 PERCENT SULFUR         7/eo
COAL   0.7 PERCENT SULFUR         7/61
 COAL   0.8 PERCENT SULFUR        10/60
 COAL  4.7  PERCENT SULFUR          4/60
 COAL    s.s- t.o PERCENT SULFUR   e/so
 COAL   0.8  PERCENT  SULFUR         4/80
 COAL  2.5-4*5 PERCENT SULFUR      6/78
 COAL    o.a- i.s PERCENT SULFUR   6/79
COAL 1.0 PERCENT SULFUR         12/78
LIGNITE - 0.63 PERCENT SULFUR   11/79
                                                               241
                                                                                           PEDCo  ENVIRONMENTAL
                                                                                                  CINCINNATI. OHIO 45246

-------
                   TABLE. 15
            SUMMARY OF PLANNED F6D SYSTEMS AS OF Ofc/77
       UTILITY COMPANY
        POWER STATION
                                 NEW OR   SIZE OF FGO  VENDOR/PROCESS
                                RETROFIT   UNIT inwi
FUEL CHARACTERISTICS
                               MO/YR
SALT RIVER PROJECT
CORONADO NO.l

SOUTHERN INDIANA GAS4ELECTRIC
A.B. BROWN NO.l

SALT RIVER PROJECT
CORONADO NO.2

TEXAS UTILITIES CO.
MARTIN LAKE NO. 4

UNITED POWER ASSOCIATION
COAL CREEK NO. 1
            LETTER OF INTENT SI6NED

NEVADA POWER
REID GARDNER NO 1

PHILADELPHIA ELECTRIC CO.
EDDYSTONE NO. IB

MINNESOTA POWER AND LIGHT CO.
CLAY BOSUELL NO. H

WISCONSIN POWER & LIGHT co.
COLUMBIA NO. 2

PUBLIC SERVICE CO OF NEW MEX.
SAN JUAN NO. 3
            REQUESTING/EVALUATING BIDS

                                    N
NORTHERN STATES POWER CO.
SHERBURNE COUNTY STATION NO.3


NORTHERN STATES POWER CO.
SHERBURNE COUNTY STATION NO.l*


TEXAS POWER ft LIGHT CO.
SANDOW N0.it


PUBLIC SERVICE OF INDIANA
GIBSON NO. H
                                    N
350
250
350
793
5*5
125
210
500
527
500
860
660
5<»5
650
PULLMAN KELLOGG
LIMESTONE SCRUBBING
FMC CORPORATION
DOUBLE ALKALI SCRUBBING
PULLMAN KELLOGG
LIMESTONE SCRUBBING
RESEARCH COTTRELL
LIMESTONE SCRUBBING
COMBUSTION ENGINEERING
LIME SCRUBBING
AOL/COMBUST ION EQUIP ASSOCIATE
SODIUM CARBONATE SCRUBBING
UNITED ENGINEERS / PECO
MAGNESIUM OXIDE SCRUBBING
PEABODY ENGINEERING
LIME/ALKALINE FLYASH SCRUBBING
CHEMICO
LIME/ALKALINE FLYASH
NOT SELECTED
REGENLRABLE NOT SELECTED
NOT SELECTED
NOT SELECTED
NOT SELECTED
NOT SELECTED
NOT SELECTED
LIMESTONE SCRUBBING
NOT SELECTED
NOT SELECTED
COAL 1.
COAL 3.
COAL 1.
COAL 1.
LIGNITE
COAL
COAL 2.
COAL 0.
COAL 0.
COAL 0.
COAL 0.
COAL 0.
LIGNITE
COAL 3.
0 PERCENT SULFUR (MAX)
75 PERCENT SULFUR
0 PERCENT SULFUR (MAX)
0 PERCENT SULFUR
- 0.63 PERCENT SULFUR
0-5- i.o PERCENT SULFUR
5 PERCENT SULFUR
6 PERCENT SULFUR
6 PERCENT SULFUR
6 PERCENT SULFUR
8 PERCENT SULFUR
8 PERCENT SULFUR

3 PERCENT SULFUR
H/79
»/79
H/80
11/82
11/78
O/ 0
6/80
0/80
1/80
1/79
5/81
5/83
7/80
0/79
                                                                                           PEDCo  ENVIRONMENTAL
                                                                                                  CINCINNATI. OHIO 4524S

-------
                   TABLE 15
            SUMMARY OF PLANNED FGO SYSTEMS AS OF 06/77
       UTILITY COMPANY
        POWER STATION
 NEW OR   SIZE OF F6D  VENDOR/PROCESS
RETROFIT   UNIT 
FUEL CHARACTERISTICS
MO/YR
PUBLIC SERVICE OF INDIANA
GIBSON NO. 3
            CONSIDERING FGD SYSTEM

LOUISVILLE GAS I ELECTRIC
MILL CREEK NO 1

NEVADA POWER
WARNER VALLEY STATION NO.  2

NEVADA POWER
WARNER VALLEY STATION NO.  1

COLUMBUS ft  SOUTHERN OHIO  ELEC.
POSTON NO.  5

NEVADA POWER
HARRY ALLEN STATION NO. 1

 NEVADA POWER
 HARRY ALLEN STATION NO. 2

 NEVADA POWER
 HARRY ALLEN STATION NO. 3

 COLUMBUS I SOUTHERN OHIO ELEC.
 POSTON NO. 6

 BASIN ELECTRIC POWER COOP
 LARAMIE RIVER NO.  3

 BASIN ELECTRIC POWER COOP
 ANTELOPE VALLEY NO. 1

 LOUISVILLE GAS 8 ELECTRIC
 MILL CREEK NO 2

 CENTRAL ILLINOIS LIGHT CO.
 DUCK CREEK NO. 2

 CINCINNATI GAS 8 ELECTRIC CO.
 EAST BEND NO 2

 BASIN ELECTRIC POWER COOP
 ANTELOPE VALLEY NO. 2
N
R
N
N
N
N
N
N
N
N
N
R
N
N
N
650
330
250
250
375
500
500
500
375
550
H50
330
too
600
450
NOT SELECTED
NOT SELECTED
NOT SELECTED
LIME SCRUBBING
NOT SELECTED
NOT SELECTED
NOT SELECTED
NOT SELECTED
NOT SELECTED
NOT SELECTED
NOT SELECTED
NOT SELECTED
NOT SELECTED
NOT SELECTED
NOT SELECTED
NOT SELECTED
NOT SELECTED
NOT SELECTED
NOT SELECTED
NOT SELECTED
NOT SELECTED
LIME/ALKALINE FLYASH SCRUBBING
NOT SELECTED
LIME SCRUBBING
NOT SELECTED
LIMESTONE SCRUBBING
NOT SELECTED
NOT SELECTED
NOT SELECTED
NOT SELECTED
                                                      COAL 3.3 PERCENT SULFUR          0/78
                                                      COAL   3.5- H.O PERCENT SULFUR   1/62
                                                      COAL                             6/83
                                                      COAL                             6/02
                                                      COAL 2.5 PERCENT SULFUR          0/61
                                                       COAL                             6/83
                                                       COAL                             6/8*
                                                       COAL                             6/85
                                                       COAL 2.5 PERCENT  SULFUR          0/83
                                                       COAL  0.8 PERCENT  SULFUR         6/83
                                                       LIGNITE  i.o  PERCENT  SULFUR        o/ai
                                                       COAL   3.5-  ».o  PERCENT  SULFUR    i/8i
                                                       COAL  2.5-3.0  PERCENT  SULFUR       1/82
                                                       COAL                             1/81
                                                       LIGNITE  i.o  PERCENT SULFUR       o/83
                                                               243
                                                                                           PEDCo  ENVIRONMENTAL
                                                                                                  CINCINNATI. OHIO 45246

-------
                    TABLE: is
             SUMMARY OF PLANNED FGO SYSTEMS AS OF 06/77
        UTILITY COMPANY
         POWER STATION
 NEW OR   SIZE OF FGO  VENDOR/PROCESS
RETROFIT   UNIT 
-------
                   TABLE 15
            SUMMARY OF PLANNED FGD SYSTEMS AS OF 06/77
       UTILITY COMPANY

        POWER STATION
TEXAS UTILITIES

FOREST 6ROVE NO. 1


PUBLIC SERVICE CO OF NEW HEX.
SAN JUAN NO. 4


SALT RIVER PROJECT
CORONADO NO.3
 NEW OR
RETROFIT
SIZE OF FGD

 UNIT inwi



   750



   500




   350
VENDOR/PROCESS
                      NOT SELECTED
                      NOT SELECTED

                      NOT SELECTED
                      REGENERABLE NOT SELECTED

                      NOT SELECTED
                      LIMESTONE SCRUBBING
 FUEL CHARACTERISTICS           MO/YR





LIGNITE                          0/81




COAL 0.6 PERCENT SULFUR          5/61




COAL 1.0 PERCENT SULFUR (MAX)     0/67
                                                              2*5
                                                                                         PEDCo  ENVIRONMENTAL

                                                                                                CINCINNATI. OHIO 45246

-------
PEDCo  ENVIRONMENTAL
     CINCINNATI. OHIO

-------
                                TABLE 16

FGD SYSTEM OPERATIONS THAT HAVE BEEN TERMINATED  OR  SHUT  DOWN  INDEFINITELY
                                                        PEDCo  ENVIRONMENTAL
                                                             CINCINNATI. OHIO 45346

-------
2<»8
                         PEDCo  ENVIRONMENTAL
                               CINCINNATI. OHIO 45246

-------
                 TABLE 16
 TERMINATED FGU SYSTEMS        06/77
IDENTIFICATION NO.


UTILITY NAME


UNIT NAME


UNIT LOCATION


UNIT RATING


FUEL CHARACTERISTICS


F6D VENDOR


PROCESS


NEW OR RETROFIT


START UP DATE


FGD STATUS


EFFICIENCY,
 PARTICULATES



 S02



WATER HAKE UP



SLUDGE  DISPOSAL



UNIT COST
ARIZONA PUBLIC SERVICE


FOUR CORNERS NO. 5A


FARHINGTON NEW MEXICO


 160 HW


COAL  0.7 PERCENT SULFUR


SO. CALIFORNIA EDISON


LIME SCRUBBING


RETROFIT


 2/76
 OPERATIONAL
 EXPERIENCE
REFER  TO THE BACKGROUND INFORMATION SECTION IN TABLE 16 OF THE REPORT.
THIS MODULE WAS ORIGINALLY INSTALLED AT THE MOHAVE GENERATING STATION
AND OPERATED DURING THE TEST MODULES EVALUATION PROGRAM. THE UNIT
WAS THEN SHUTDOWN* MOVED FROM THE MOHAVE TEST SITE. AND REASSEMBLED
AT THE FOUK CORNERS STATION OF APS. THE MODULE WAS IN SERVICE DURING
SEGMENTS FROM FEB. 1976 TO DEC. 6« 1976. TREATING APPROXIMATELY 20 PER-
CENT OF THE FLUE GAS FLOW FROM THE 755-MW RATED UNIT. THE PROGRAM HAS
BEEN TERMINATED AND THE MODULE DISASSEMBLED.
                                                           249
                                                                                       PEDCO  ENVIRONMENTAL-


                                                                                              CINCINNATI. OHIO  452.46

-------
                                                      BACKGROUND INFORMATION

                                                                ON

                                      FOUR CORNERS NO. 5A - EXPERIMENTAL HORIZONTAL SCRUBBER

     THE FOUR CORNERS POWER STATION. LOCATED NEAR FARMINGTON.  NEW MEXICO. IS JOINTLY OWNED BY THE ARIZONA PUBLIC SERVICE COMPANY

AND THE SOUTHERN CALIFORNIA EDISON COMPANY.  THIS STATION CONTAINS FIVE COAL-FIRED BOILERS WITH AN EQUIVALENT ELECTRIC POWER

GENERATING CAPACITY OF 2233-MU.  ONLY UNIT NO. 5 IS RETROFITTED WITH AN FGD SYSTEM.

     UNIT NO. 5 IS A COAL-FIRED BOILER CAPABLE OF GENERATING 5.1H6.000 LBS. OF STEAM. WHICH IS EQUIVALENT TO 600-MW OF NET ELEC-

TRICAL POWER.  THIS UNIT WAS FIRST PLACED IN COMMERCIAL OPERATION JULY 1970. APPROXIMATELY 20 PERCENT OF THE FLUE GAS GENERATED BY

THIS BOILER IS BEING SCRUBBED INITIALLY IN ORDER TO ESTABLISH WHAT SULFUR DIOXIDE AND PARTICULATE REMOVAL EFFICIENCIES CAN BE

OBTAINED.

     THE FGO SYSTEM WHICH HAS BEEN RETROFITTED ON UNIT NO. 5 IS THE WEIR HORIZONTAL CROSSFLOW SPRAY SCRUBBER WHICH WAS FORMERLY

INSTALLED AND OPERATED IN A TEST PROGRAM AT THE MOHAVE GENERATING STATION OF THE SOUTHERN CALIFORNIA EDISON COMPANY(SEE MOHAyE NO.

2A IN TABLE 16 OF THIS REPORT I.

     DURING THE MOHAVE TEST PROGRAM THE HORIZONTAL MODULE WAS OPERATIONAL FROM NOVEMBER It 1973. TO JANUARY 16.197H, FOR SHAKEDOWN

PURPOSES.  OVER THE COURSE OF THE ACTUAL TEST PROGRAM. WHICH EXTENDED FROM JANUARY 16, 197H. TO FEBRUARY 9, 1975. THE PROTOTYPE

UNIT OPERATED A TOTAL OF 5,927 HOURS IN VARIOUS TEST MODES.  FOLLOWING COMPLETION OF TESTS. THE MODULE WAS SHUT DOWN. DISMANTLED*

TRANSPORTED, AND REASSEMBLED AT THE FOUR CORNERS GENERATING STATION OF ARIZONA PUBLIC SERVICE FOR FURTHER TESTING.

     THE HORIZONTAL MODULE IS A FOUR-STAGE SCRUBBING CHAMBER WITH THE FOLLOWING DIMENSIONS*  LENGTH - H8 FEET* WIDTH - 26 FEET*

HEIGHT - 15 FEET.  THE MODULE ITSELF IS A HOLLOW CHAMBER CONSISTING OF FOUR STAGES OF CROSSFLOW SPRAY NOZZLES. EACH STAGE CONTAIN

A ROW OF 36 EXTERNALLY-MOUNTED NOZZLES.  THE SLURRY IS CYCLED THROUGH THE SCRUBBER IN A COUNTERCURRENT MANNER AT A RATE OF 36,000

GPM/STAGE.  FRESH LIME SLURRY IS SPRAYED ACROSS THE FLUE GAS AT THE FOURTH STAGE, WHICH IS THE DISCHARGE END OF THE SCRUBBING

CHAMBER.  THE SCRUBBING SOLUTION IS THEN COLLECTED AND RECYCLED SUCCESSIVELY TO THE THIRD,SECOND,AND FIRST STAGES OF THE SCRUBBING

MODULE.  THIS ALLOWS FOR COMPLETE DEPLETION OF ANY EXCESS ALKALINITY AND INSURES THAT FRESH SLURRY IS CONTACTING GAS HAVING THE

LOWEST SUFLUR DIOXIDE CONCENTRATION.  THE LIQUID RECIRCULATION RATE CAN BE ADJUSTED OyER A WIDE RANGE.  THE MODULE IS DESIGNED TO

TREAT A MAXIMUM FLUE GAS CAPACITY OF <»50«000 SCFM.  THE DESIGN GAS VELOCITY THROUGH THE MODULE IS 21.6 FT./SEC.  THE CLEANED GASES

THEN PASS THROUGH A DEHISTER AND ARE REHEATED BEFORE BEING DISCHARGED TO THE STACK.  THE SPENT SLURRY IS DISCHARGED FROM THE
                                                               250

                                                                                           PEDCo  ENVIRONMENTAL
                                                                                                 CINCINNATI. OHIO

-------
FOUR CORNERS NO. 5A (CONTINUEEDI

SCRUBBING SYSTEM TO A THICKENER AND THE UNDERFLOW IS  PUMPED  TO  AN ON-SITE SETTLING POND.  WATER IS RETURNED TO THE PROCESS FOR

FURTHER USE.

     A CUTAWAY VIEW OF THE WEIR SCRUBBING CHAMBER IS  PRESENTED  IN APPENDIX B.
                                                               251
                                                                                           PEDCo  ENVIRONMENTAL
                                                                                                  CINCINNATI. OHIO 45246

-------
                                                   FOUR CORNERS  NO.  5A
                   OPtRATlNG HOURS
PERIOD        BOILER         F&O SYSTEM
MONTH/YEAR
FEB. 76

MAR. 76
APR. 76
HAT  76
JUN. 75
JUL. 76
AUG. 76
SEP. 76
OCT. 76
NOV. 76
DEC. 76
                             COMMENTS
INSTALLATION OF THE MODULE AT THE FOUR CORNERS GENERATING STATION WAS
COMPLETED AND THE MODULE WAS PLACED IN-SERVICE FEBRUARY 17i 1976i
FOR INITIAL OPERATION.
THE SYSTEM WAS TAKEN DOWN IN MID-APRIL FOR A SCHEDULED BOILER OVERHAUL.
SYSTEM RESTART IS SCHEDULED FOR JULY 1976.

THE SYSTEM HAS REMAINED OUT OF SERVICE SINCE MID-APRIL 1976 BECAUSE OF AN
EXTENSIVE OVERHAUL TO THE NO. 5 BOILER PLUS THE DEVELOPMENT OF PROBLEMS
WITH THE SCRUBBER MODULE'S REHEATER UNIT.

THE PROTOTYPE WAS IN SERVICE THROUGHOUT THE MONTH OF NOVEMBER. ON DEC.6 THE TEST
PROGRAM WAS CONCLUDED AND THE UNIT HAS SINCE BEEN DISMANTLED.  APS IS NOW IN THE
PROCESS OF ANALYZING THE OPERATING DATA ACCUMULATED DURING THE TEST PERIOD. A
REPORT ADDRESSING THE RESULTS OF THE PROGRAM WILL BE PUBLISHED IN FEBRUARY 1977.
                                                               252
                                                                                           PEDCo  ENVIRONMENTAL
                                                                                                  CINCINNATI. OHIO  U5246

-------
                 TABLE 16
 TERMINATED FGU SYSTEMS
          06/77
IDENTIFICATION NO.
UTILITY NAME
UNIT NAME
UNIT LOCATION
UNIT RATING
FUEL CHARACTERISTICS
FGD VENDOR
PROCESS
NEW OR RETROFIT
START UP DATE
FGD STATUS
EFFICIENCY*
 PARTICULATES

 S02

WATER HAKE UP

SLUDGE  DISPOSAL
UNIT COST
 OPERATIONAL
  EXPERIENCE
BOSTON EDISON
MYSTIC NO b
EVERETT  MASSACHUSETTS
  iso  nu
OIL   2.5 PERCENT SULFUR
CHEMICO
MAGNESIUM OXIDE SCRUBBING
RETROFIT
  «/72


50 PERCENT

90 PERCENT
SJ2/KW CAPITAL * CALCINATION
 AVERAGE FGD SYSTEM AVAILABILITY  FACTORS  -  APRIL  72  TO  MAY  73.  17*.
 JUNE 73 TO DEC* 73. 481.   JAN. 7>»  TO  JUNE  7t.  60*.  JUNE  74*  BOX.
 THE FGO SYSTEM HAS BEEN SHUT  DOWN  INDEFINITELY SINCE JUNE  74.
                                                           253
                                                                                       PEDCp  ENVIRONMENTAL
                                                                                              CINCINNATI. OHIO 45246

-------
     THE MAGNESIUM OXIDE-BASED FGD SYSTEM INSTALLED AT THE MYSTIC POWER STATION OF THE BOSTON EDISON COMPANY CONSISTS OF A CHEH-
KO-DESIGNED SINGLE-STAGE VENTURI SCRUBBER MODULE.   THE MODULE IS CONSTRUCTED OF CARBON STEEL LINED WITH A SPRAY-APPLIED POLYEST-
ER MATERIAL.  TOTAL FLUE GAS CAPACITY OF THE SYSTEM IS 
-------
MONTH/YR
APR.
TO
HAY
JUN.
JUL.
AUG.
SEP.
OCT.
NOV.
DEC.
JAN.
FEB.
MAR*
APR.
MAY
JUN.
72

73
73
73
73
73
73
73
73
7*
7«»
7«»
74
7«»
7«f
BOILER
OPERATION
(HR»



592
575
BOILER
637
627
629
658
555
5*1
*oa
585
488
559
SCRUBBER
OPERATION
(HR)



102
351
SHUTDOWN
243
377
162
86
152
138
353
471
280
288
OPERABILITY IK)
17


68
61

38
60
26
13
28
25
87
81
57
80
      srsrcn AVAILABILITY

      MYSTIC UNIT NO. b
                                    COMMENTS

THE MODULE OPERATED INTERMITTENTLY BECAUSE OF MECHANICAL DIFFICULTIES.  A MAJOR

PROBLEM CONCERNED THE OPERATION OF THE MAGNESIUM SULFITE CRYSTALS DRYER.



THE LONGEST PERIOD OF CONTINUOUS OPERATION. 7.5 DAYS. OCCURRED DURING JUNE AND

JULY.

THE BOILER WAS DOWN FOR THE ANNUAL OVERHAUL.  SYSTEM AVAILABILITY DECREASED

DURING THE LAST QUARTER OF THE YEAR BECAUSE OF HEAVY EROSION/CORROSION IN THE

LIQUOR RECIRCULATION PUMPS AND CENTRIFUGE.
SYSTEM AVAILABILITY WAS LIMITED BY BOILER-RELATED PROBLEMS THAT CAUSED FREQUENT

SHUTDOWNS IN JANUARY AND FEBRUARY.



TWO 7-DAY CONTINUOUS OPERATION PERIODS OCCURRED DURING THE MONTH.

THE 57 PERCENT OPERABILITY INDEX VALUE FOR THE MONTH WAS DUE TO A 2-WEEKS OUT-

AGE OF THE ACID PLANT RATHER THAN TO FGD SYSTEM FAILURE.  DEMONSTRATION PRO-

GRAM WAS COMPLETED AND FGD SYSTEM WAS SHUT DOWN.  EPA FUNDING OF MGS03 CALCIN-

ATION HAS EXPIRED.  THERE ARE NO DEFINITE PLANS FOR RESTARTING OF THIS UNIT.

MAJOR PROBLEM AREAS ENCOUNTERED DURING THE OPERATION OF THIS PROTOTYPE UNIT

INCLUDED TRIHYDRATE INSTEAD OF HEXAHYDRATE SULFITE CRYSTAL FORMATION, OUST

PROBLEMS IN THE DRYER. LACK OF STACK GAS REHEAT CAUSING CONDENSATION IN THE

STACK. LOUVER DAMPER PROBLEMS. EROSION OF PUMPS. PIPING. AND CENTRIFUGE. AND

MINOR ANCILLARY EQUIPMENT FAILURES.
            255
                                       PEDCo  ENVIRONMENTAL
                                              CINCINNATI. OHIO 45246

-------
                 TABLE 16
 TERMINATED FGD SYSTEMS
          06/77
IDENTIFICATION NO.
UTILITY NAME
UNIT NAME
UNIT LOCATION
UNIT RATING
FUEL CHARACTERISTICS
F60 VENDOR
PROCESS
NEW OR RETROFIT
START UP DATE
FGD STATUS
EFFICIENCY.
 PARTICULATES
 S02
WATER HAKE UP
SLUDGE DISPOSAL
UNIT COST
OPERATIONAL
 EXPERIENCE
 CENTRAL ILLINOIS LIGHT CO,

 DUCK CHEEK NO. 1A

 CANTON ILLINOIS

  100 MW

 COAL 2.5 - 3.0 PERCENT SULFUR

 RILEY STOKER / ENVIRONEERING

 LIMESTONE SCRUBBING

 NEW

  9/76




 99.8 PERCENT
 75 PERCENT


 CLOSED LOOP


 UNSTABILIZED SLUuGE DISPOSED IN LINED POND


$80/KW CAPITAL (ESTIMATED)
 THE INSTALLATION OF ONE OF A TOTAL OF FOUR SCRUBBER MODULES WAS
 COMPLETED IN JULY 1976 AND START-UP OPERATIONS COMMENCED. SHAKEDOWN
 AND DEBUGGING OPERATIONS PROCEEDED ON AN INTERMITTENT BASIS
 BECAUSE OF NUMEROUS CHEMICAL AND MECHANICAL-RELATED PROBLEMS.
 THE SINGLE COMPLETED SCRUBBER MODULE HflS BEEN SHUTDOWN UNTIL THE OTHER
 THREE MODULES. REPRESENTING 300 MW OF SCRUBBING CAPACITY. ARE READY IN
 AUGUST 1978. UNTIL THAT TIME THE «»00-MW UNIT WILL BE UTILIZING COLORADO
 LOW-SULFUR COAL FOR POWER GENERATION OPERATIONS.
                                                           256
                                                                                        PEDCo  ENVIRONMENTAL
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                                                      BACKGROUND INFORMATION
                                                                ON
                                                      DUCK CREEK PLANT NO 1A
     THE DUCK CREEK PLANT OF THE CENTRAL ILLINOIS LIGHT COMPANY (CILCO) IS A NEW COAL-FIRED POWER-GENERATING STATION LOCATED IN
AN UNRECLAIMED STRIP-MINING AREA NEAR CANTON, ILLINOIS.  AT THE PRESENT TIME, ONE HOO-MW COAL-FIRED UNIT IS IN SERVICE AND THREE
MORE IDENTICAL UNITS ARE BEING PLANNED. BRINGING THE TOTAL PLANNED PLANT CAPACITY TO 2000 HW.
     THE NO. 1 POWER-GENERATING UNIT INCLUDES A 3-MILLION LBS./HR. STEAM-GENERATING BOILER (2600 PSlGt 1005F/1005F, SINGLE REHEAT,
PULVERIZED-COAu-FIREO. BALANCED DRAFT) SUPPLIED BT THE RlLEY STOKER CORPORATION TO PROVIDE STEAM TO «»00-MW TURBINE.  THE BOILER
IS DESIGNED TO FIRE HIGH-SULFUR ILLINOIS COAL, AVAILABLE FROM NEARBY MINES, HAVING THE FOLLOWING AVERAGE CHARACTERISTICS*  HEAT
CONTENTt 10«500 BTU/LB* SULFUR CONTENT 2>*t TO <>.0 PERCENT* ASH CONTENT, 6.0 TO 16.0 PERCENT.  CONSTRUCTION OF THE NO. 1 UNIT BEGAN
IN THE EARLY PART OF 1972. COMMERCIAL SERVICE COMMENCED IN JUNE 1976.
     THE DESIGN OF THE EMISSION CONTROL SYSTEM FOR THIS UNIT CONSISTS  OF TWO H9.6 PERCENT-EFFICIENT ELECTROSTATIC PRE-
CIPITATORS SUPPLIED BT POLLUTION CONTROL-WALTHER  (PCW) FOR THE CONTROL OF PARTICULATES AND FOUR WET-LIMESTONE SCRUBBER MODULES
SUPPLIED BY RILET STOKER/ENVIRONEERING FOR THE REMOVAL OF 75 PERCENT OF THE SULFUR DIOXIDE.   THE EMISSION CONTROL SYSTEM IS DE-
SIGNED TO FUNCTION IN THE FOLLOWING MANNER*   THE  BOILER FLUE GAS,  AFTER PASSING THROUGH  TWO AIR PREHEATER UNITS, ENTERS THE PCW
ESP'S WHERE PRIMARY PARTICULATE REMOVAL OCCURS.   THE PARTICULATE-CLEANED GAS IS THEN DISCHARGED TO A MANIFOLD SUPPLYING FOUR CEN-
TRIFUGAL INDUCED DRAFT FANS  (RADICAL  TIP,  INLET-DAMPER CONTROL, 900 RPM, <>000 HP EACH).  THE  FLUE GAS IS BOOSTED THROUGH A COMMON
HEADER  INTO THE 4-HODULE  SCRUBBER  PLANT.   EACH VENTURI-ABSORBER MODULE IS EQUIPPED WITH  INLET/OUTLET DAMPERS SO THAT GAS CAN BE
ROUTED  AROUND  ONE  OR  ALL  THE MODULES  THROUGH BY-PASS BREECHING TO  THE  MAIN STACK.  SULFUR DIOXIDE IS REMOVED FROM THE FLUE GAS IN
COUNTERCURRENT FASHION VIA  LIMESTONE  SLURRY  SPRAYED ON THE ROD SECTIONS IN THE ABSORBER  MODULES.  THE LIMESTONE REAGENT IS STORED
ON  THE  PLANT SITE  AND PREPARED IN  SLURRY FORM VIA GRINDING IN A HO TPH WET BALL MILL.  THE PRODUCT OF THE MILL SYSTEM, A 35 TO 
-------
DUCK CREEK PLANT NO 1A (CONTINUED)

TO THE PLANT FOR REUSE IN THE ASH  AND S02-REMOVAL SYSTEMS.

CURRENT STATUS*  CONSTRUCTION OF THE  NO.1  UNIT COMMENCED IN THE EARLY PART OF 1972 AND WAS VIRTUALLY COMPLETED BY THE SPRINB OF

1976.  COMMERCIAL OPERATION COMMENCED IN JUNE 1976 WITH THE ESP MODULES IN THE 6AS PATH.  THE FIRST MODULE OF THE FOUR-MODULE

SCRUBBER PLANT WAS INSTALLED BY JUNE  1976  AND START-UP FOR  SHAKEDOWN AND DEBUGGING PURPOSES OCCURRED IN JULY.  ONE MODULE IS

CAPABLE OF TREATING THE EQUIVALENT OF APPROXIMATELY 100-MW  OF BOILER FLUE GAS.  THE REMAINING THREE MODULES OF THE SCRUBBER

PLANT ARE NOW BEING INSTALLED.  INITIAL OPERATION OF THE SCRUBBING SYSTEM WITH ALL FOUR MODULES IN THE GAS PATH IS SCHEDULED FOR

AUGUST 1. 1978.  A SIMPLIFIED PROCESS FLOW DIAGRAM OF THE. DUCK CREEK NO. 1 EMISSION CONTROL SYSTEM IS PROVIDED IN

APPENDIX B.  ADDITIONAL INFORMATION ADDRESSING THE INITIAL  OPERATION OF THE NO.i MODULE IS PROVIDED IN THE PERFORMANCE TABLE THAT

FOLLOWS.
                                                               258
                                                                                            PEDCo  ENVIRONMENTAL
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PERIOD

JULY 76
   MODULE
OPERATION, HRS.

    8 MRS.
AUG. 76
   18 HRS.
SEP. 76
  360 HRS.
OCT. 76
  385 HRS.
NOV. 76
  20 HRS.
          DUCK CHEEK NO.14* PERFORMANCE HISTORY


                         COMMENTS

INITIAL OPERATION OF THE FIRST SCRUBBER MODULE FOR SHAKEDOWN

AND DEBUGGING PURPOSE OCCURED DURING THE MONTH.  LIMITED SERVICE

TIME RESULTED FROM PROBLEMS WITH BAD WELDS. FAULTY PIPE MANGES.

AND ABSORBER LEAKS.

LIMITED OPERATIONS CONTINUED THROUGHOUT AUGUST BECAUSE OF THE

START-UP AND CONSTRUCTION PROBLEMS MENTIONED ABOVE.  THE MODULE WAS

TAKEN OUT OF THE GAS PATH AT THIS POINT TO CONCENTRATE ON RESOLVING

THESE PROBLEM AREAS.

MODULE RESTART OCCURRED ON SEPT. 9,  OPERATION CONTINUED THROUGHOUT

THE REMAINDER OF THE MONTH ON AN INTERMITTANT BASIS.  MAJOR PROBLEMS

INCLUDED PIPE BREAKING. PUMP LINER FAILURES, PLUGGING AND SEALING

OF MIST ELIMINATORS, AND SOME BOILER-RELATED PROBLEMS.  THE MODULE

REMAINED IN SERVICE FOR APPROXIMATELY is DAYS OF NON-CONTINUOUS

OPERATION.  THE PCW ESP MODULES HAVE REMAINED IN SERVICE WITHOUT THE

OCCURRANCE OF ANY MAJOR PROBLEMS.

TOTAL OPERATION TIME DURING THE MONTH WAS APPROXIMATELY 16 DAYS

(NON-CONTINUOUS).  MAJOR PROBLEM AREA WAS THE CONTINUATION OF MASSIVE

SCALE DEVELOPMENT ON THE MIST ELIMINATORS, RESULTING IN PLUGGING OF

THE PIPING AND NOZZLES TO THE COMPONENTS SPRAY SYSTEM.

SPORADIC OPERATION RESULTED FROM CONTINUED SCALING PROBLEMS IN THE

MIST ELIMINATOR SECTION.  RILEY AND CILCO INITIATED MODIFICATIONS TO

THE DESIGN OF THE MODULE.  SPECIFICALLY, A ROD DECK WAS CHANGED IN

THE ABSORBER, PRESSURE DROP ACROSS THE ABSORBER WAS INCREASED,

PIPING AND PUMP LINER MATERIALS WERE MODIFIED/REPLACED, AND A FRESH

WATER WASH SYSTEM WAS INSTALLED FOR THE MIST ELIMINATOR.
                                                               259
                                                                                            PEDCo ENVIRONMENTAL.
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              MODULE
PERIOD     OPERATION,  MRS.
DEC. 76
JAN. 77
FEB. 77


MAR. 77      350 MRS.
    DUCK CREEK NO. 1A* PERFORMANCE HISTORY (CONTINUED)
                         COMMENTS
THE MODULE REMAINED OUT OF SERVICE THE ENTIRE MONTH.  DURING THIS
TIME, THE BOILER FIRED LOW SULFUR (0.6K) KENTUCKY COAL.
TH£ NO. 1 UNIT UAS DOWN THROUGHOUT THE ENTIRE PERIOD FOR TURBINE/
BOILER OVERHAUL.  DURING THE UNIT OUTAGE, A NUMBER OF MODIFICATIONS
WERE MADE TO THE SCRUBBER.
THE NO. 1 UNIT WAS RETURNED TO SERVICE IN MID-MARCH.  THE SCRUBBER WAS
PLACED IN SERVICE TO TEST THE MODIFICATIONS MADE DURING THE PRECEDING
OUTAGE.  THESE MODIFICATIONS INCLUDED*
* THE. MIST ELIMINATOR SPKAY WASH SYSTEM PIPING WAS CHANGED FROM PVC TO
  FRP MATERIALS.  ALSO, AN ADDITIONAL SPRAY HEADLR WAS ADDED.
* THt SLURRY CIRCULATION SYSTEM WAS RLVAMPEU.
* NEOPRENE PUMP LINERS HAVE REPLACED THE ORIGINAL RUBBER LINERS.  FLUSH/
  DRAIN SYSTEMS HAVE BEEN INCLUDED TO MINIMIZE SOLIDS BUILD UP,
* PIPING VALVES *OVEO CLOSER TO THE KECYCLE TANK.
« SLURRY STORAGE  TANKS EQUIPPED WITH FLUSH/DRAIN SYSTEMS.
* ADDITIONAL MIXERS ADDED FOR GREATER AGITATION TO PROMOTE PROCESS
  CHEMISTRY.
DURING THE LAST PART OF MARCH THE MODULE REMAINED IN SERVICE ON A CON-
TINUAL BASIS WITH THE EXCEPTION OF A FEW MINOR BOILER OUTAGES.  CILCO
INTENDS TO CONTINUE EXPERIMENTAL OPERATIONS THROUGHOUT THE APRIL-MAY
PERIOD, TESTING THE MECHANICAL MODIFICATIONS AND THE AUTOMATIC CONTROL
LOOPS (SYSTEM CHEMISTRY WILL BE CONTROLLED BY INLET/OUTLET 803 LOADING.
SOLUTION PH, SOLUTION SOLIDS.  OPERATION UP TO THIS POINT HAS PROCEEDED
IN A MANUAL CONTROL MODE).  CONTINUED OPERATION BEYOND THIS TIME FRAME
WILL DEPEND UPON THE SUCCESS OF EXPERIMENTAL OPERATIONS.  CILCO HAS THE
                                                               2foU
                                                                                           PEDCo  ENVIRONMENTAL
                                                                                                 CINCINNATI. OHIO 452.46

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PERIOD
APR. 77

MAY  77
   MODULE
OPERATION. MRS.
    UUCK CRECK NO. 1A* PERFORMANCE HJSTORf {CONTINUED!



                         COMMENTS


OPTION OF FIRING LOW SULFUR  COAL UNTIL  THE ENTIRE H-MOOULE SCRUBBER PLANT


IS READY FOR SERVICE IN AUGUST  197S.

THE UNIT CONTINUED TO FIRE LOW-SULFUR COLORADO COAL DURING THE REPORT PERIOD. THE RESTART OF


SCRUBBER OPERATIONS CONTINUES TO BE SCHEDULED FOR AUGUST 1976
                                                               261
                                                                                          PEDCo  ENVIRONMENTAL.
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                 TABLE 16
 TERMINATED FGO SYSTEMS
         06/77
IDENTIFICATION NO.
UTILITY NAME
UNIT NAME
UNIT LOCATION
UNIT RATING
DAIRYLAND POHE« COOP

ALMA STATION

ALMA WISCONSIN

  60 MW
FUEL CHARACTERISTICS  COAL   3.0-3.5 PERCENT SULFUR
FGD VENDOR

PROCESS

NEW OR RETROFIT

START UP DATE

FGD STATUS

EFFICIENCY.
 PARTICULATES
FOSTER WHEELER

LIME INJECTION

RETROFIT

 6/71
 S02
25 PERCENT
WATER HAKE UP
SLUDGE DISPOSAL
UNIT COST
OPERATIONAL
 EXPERIENCE
THIS EXPERIMENTAL WET LIME FuRNACE SYSTEM BEGAN OPERATIONS IN '71 AND WAS
OPERATIONAL FOK PERIODS UP TO 30 DAYS. IN AUGUST 1971* THE UNIT WAS TESTED
FOR TWO DAYS USING WESTERN LOW-SULFUR COAL. THE TEST SHOWED ABOUT SOX
S02 KEHOVAL EFFICIENCY. BUT PRECIPITATOK PERFORMANCE WAS ADVERSELY
AFFECTED.  THE FGD PROJECT HAS BEEN SHUT DOWN INDEFINITELY SINCE
AUGUST 197*. AND THERE AKE NO PLANS FOR FUTURE OPERATION.
                                                           262
                                                                                        PEDCo  ENVIRONMENTAL
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                 TABLE 16
 TERMINATED FGD SYSTEMS
         06/77
IDENTIFICATION NO.
UTILITY NAME
UNIT NAME
UNIT LOCATION
UNIT RATING
FUEL CHARACTERISTICS
F6D VENDOR
PROCESS
NEW OR RETROFIT
START UP DATE
FGO STATUS
EFFICIENCY!
 PARTICULATES

 S02

WATER MAKE  UP

SLUDGE  DISPOSAL

UNIT COST
 OPERATIONAL
  EXPERIENCE
DETROIT EDISON
ST. CLAIR NO 6
BELLE RIVER MICHIGAN
  163 MW
COAL 0.3 PERCENT  SULFUR
PEABODY ENGINEERING
LIMESTONE SCRUBBING
RETROFIT
  5/76


99.7 PERCENT

90 PERCENT

 OPEN LOOP 1.07 GPM/MW

 UNSTAalLIZED SLUU6E DISPOSED IN LINED POND

S92/KU CAPITAL * 2.4 MILLS/KWH OPERATING
 REFER TO THE BACKGROUND INFORMATION SECTION IN TABLE 16 OF THIS REPORT.
 FOLLOWING THE COMPLETION OF A TWO MONTH INTERNAL S02 SCRUBBING DEMONSTRA-
 TION PROGRAM THE SCRUBBER PLANT WAS BYPASSED.  MODIFICATIONS ARE BEING
 IMPLEMENTED TO OPERATE IN THE PARTICIPATE MODE ONLY. VENTURI SCRUBBERS
 FOR PARTICIPATE REMOVAL WILL BE PUT IN OPERATION IN SEVERAL MONTHS.  SPRAY
 TOWERS WILL NOT BE USED AS ORIGINALLY  PLANNEU. THE BOILER IS NOW FIRING
 LOW-SULFUR (0.3 PERCENT) WESTERN (DECKER) COAL.  COMPLIANCE WITH S02
 REGULATIONS IS BEING ACHIEVED WITHOUT  THE NECESSITY OF SCRUBBING.
                                                           263
                                                                                      PEDCo  ENVIRONMENTAL
                                                                                             CINCINNATI. OHIO 45246

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                                                      BACKGROUND INFORMATION

                                                                ON

                                                         ST. CLAIR NO. 6

      THE ST. CLAIR POWER PLANT OF THE DETROIT EDISON COMPANY IS LOCATED ON THE ST. CLAIR RIVER IN BELLE RIVER. MICHIGAN. APPROXI-

 MATELY 45 MILES NORTHEAST OF DOWNTOWN DETROIT.  THIS PLANT CONTAINS 7 FOSSIL-FUEL-FIRED GENERATING UNITS WHICH HAVE A TOTAL NET

 GENERATING CAPACITY OF 1775-MW.  UNIT NO.  & IS A COAL-FIRED TWO-STAGE SUPERHEATER UNIT* CONTAINING TWO SEPARATE BOILER BOXES KNOWN

 AS THE SOUTH BOILER AND THE NORTH BOILER.   THE TOTAL NET GENERATING CAPACITY OF THE NO. 6 UNIT IS 325 MW.  THE SUPERHEATER WAS

 MANUFACTURED BY COMBUSTION ENGINEERING AND PLACED IN SERVICE IN 1961.  BOTH THE NORTH BOILER AND THE SOUTH BOILER ARE EQUIPPED

 WITH EMISSION CONTROL SYSTEMS. THE UNIT CURRENTLY OPERATES AT EXCESS AIR RATES OF 115 TO 120 PERCENT.

     THE ST.CLAIR NO.6 BOILER FIRES EXCLUSIVELY A LOW SULFUR WESTERN SUBBITUMINOUS COAL ORIGINATING FROM THE DECKER COMPANY'S

 DIETZ MINE LOCATED IN SOUTHERN MONTANA. THE AVERAGE CHARACTERISTICS OF THIS COAL ARE* HEAT CONTENT 9900 TO 9600 BTU/LB*SULFUR CON-

 TENT OF 0.3 TO O.t PERCENT* ASH CONTENT OF «».0 PEKCENT* AND A TOTAL MOISTURE CONTENT OF 22.0 TO 2*».0 PERCENT.

     THE EMISSION CONTROL SYSTEM INSTALLED ON THE NORTH BOILER CONSISTS OF MECHANICAL COLLECTORS AND AN ELECTROSTATIC PRECIPITATOR

 
-------
                                                      FGD SYSTEM PERFORMANCE
                                                         ST. CLAIR NO. 6
PERIOD                                                       COMMENTS
NOV. 71             INSTALLATION OF THE FGD SYSTEM WAS ESSENTIALLY COMPLETED BY THIS TIME.  A FAULTY  INSTRUMENT PANEL WHICH WAS
DEC* 7«»             INCORRECTLY WIRED HAS BEEN RETURNED TO THE MANUFACTURER FOR REPAIR.  TO DATE, THE UTILITY HAS WATER TESTED ALL
JAN. 75             THE AUXILIARY EQUIPMENT.  THE I.D. FAN HAS BEEN TESTED AND AIR BALANCE HAS BEEN CHECKED.
FEB. 75
MAR. 75             A COLD FLUE 6AS RUN WAS SUCCESSFULLY CONDUCTED MARCH  22 TO 25.  DURING THIS  PERIOD*  THE  RUBBER-LINED  PUMPS
APR. 75             WERE  REPAIRED AND THE LIMESTONE  PREPARATION  SYSTEM WAS CALIBRATED.
MAY 75
JUN.  75              THE FIRST HOT FLUE  6AS  RUN WAS  CONDUCTED ON  JUNE  22,  1975.   THE  RUN LASTED FOR  A  PERIOD  OF  22 HOURS.   DURING
JUL.  75              THIS RUN, THE SCRUBBER  WAS PURPOSELY TRIPPED OFF  AT LOADS OF tO  AND 80  PERCENT.   THIS WAS PERFORMED TO OBSERVE
                     IF ANY DETRIMENTAL EFFECTS TO THE STEAM GENERATION OPERATIONS RESULTED.   NONE WERE DETECTED.   THE SYSTEM  WAS
                     TAKEN OUT OF SERVICE FOLLOWING THIS GAS RUN TO CORRECT THE FOLLOWING MAJOR OPERATION AREAS*
                          GAS CIRCUIT*  LURGI THROAT POSITIONAL FAILURE* DETERIORATION OF THE DAMPER SEALS* SEVERE DUCT VIBRATIONS*
                          S02 ANALYZERS INOPERATIVE.
                          LIQUID CIRCUIT*  FAILURE OF PH CONTROL SYSTEM* TARGET FLOW METER TARGETS HAVE BEEN BROKEN OFF* PUMP  SEAL
                          WATER LOU FLOW ALARM TRIPS.
 AUG. 75             A  SECOND HOT FLUE GAS RUN WAS INITIATED ON AUGUST 6 AND LASTED 27 HOURS.  THE RUN WAS TERMINATED BECAUSE  OF A
                     REHEATER THERMOCOUPLE FAILURE*  A SUBSEQUENT INSPECTION OF THE SCRUBBING SYSTEM REVEALED NO APPARENT ABNOR-
                     MALITIES OR MALFUNCTIONS.
 SEP. 75
 OCT. 75             A  THIRD HOT FLUE GAS RUN OF m HOURS DURATIONWAS COMPLETED OCTOBER 9.   THE MAIN OBJECTIVE OF  THIS RUN WAS TO
                     EVALUATE VARIOUS COMPONENTS OF THE FRESH WATER SPRAY SYSTEM AND  EFFECTS ON SYSTEM OPERATION.   THE TEST RUN WAS
                     PREMATURELY TERMINATED BECAUSE OF A BOILER FEED PUMP MALFUNCTION,  RESULTING IN  A  REDUCED BOILER LOAD
                     CAUSING SUBSEQUENT WEEPING OF THE WASH TRAY.
                                                                                            PEDCo  ENVIRONMENTAL
                                                                                                   CINCINNATI. OHIO 45246

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                                                FGD  SYSTLH PERFORMANCE  tCONTINUEDl
                                                         STi  CLAIK  NO.  6
PERIOD                                                       COMMENTS
NOV. 75
DEC. 75             « FOURTH FLUE GAS RUN OF 23 OATS DURATION WAS TERMINATED  DUE  TO  EXCESSIVE  VIBRATION  IN  THE  I.D.  BOOSTER FAN.
                    ONE OTHER SCRUBBER-RELATED OUTAGE OCCURRED WHEN THE PACKING OF ONE  OF  THE  SCRUBBER RECIRCULATION PUMPS NEEDED
                    MAINTENANCE.  S02 REMOVAL DURING THIS PERIOD MAS 90 PERCENT AND  PARTICIPATE  OUTLET LOADING  WAS  0.1  LB/1000 LBs
                    OF FLUE GAS FOR 1 TO 3 PERCENT SULFUR COAL.
JAN. 76
FEB. 76
MAR. 76
APR. 76             THE 30-DAY VENDOR QUALIFICATION  RUN AND FINAL ACCEPTANCE  TESTS  WERE COMPLETED BY MAY 29.  THE QUALIFICATION
NAY  76             RUN WAS CONDUCTED ON A *HANDS OFF* BASIS USING PLANT  PERSONNEL  EXCLUSIVELY.   THE SYSTEM HAS IN  SERVICE 100
                    PERCENT OF THE TIME THE BOILER WAS OPERATIONAL.  THE  FINAL ACCEPTANCE  TEST CONSISTED OF SIX H-HR. TEST RUNS
                    CONDUCTED IN THE SPACE OF ONE WEEK.  THE S02 REMOVAL  EFFICIENCY  FOR HIGH SULFUR COAL WAS  90.9 PERCENT.
                    PARTICULATE REMOVAL ALSO EXCEEDED DESIGN LEVELS.  NO  MAJOR MECHANICAL  OR CHEMICAL-RELATED PROBLEMS WERE
                    ENCOUNTERED.
JUN. 76
JUL. 76
AUG. 76             THE UTILITY IS NOW PREPARING TO  CONDUCT A 2 MONTH  MINIMUM INTERNAL  SCRUBBER  DEMONSTRATION PROGRAM TO ACQUIRE
                    OPERATING DATA AND INFORMATION.   FOLLOWING THE COMPLETION OF  THIS PROGRAM THE BOILERS WILL  FIRE LOw SULFUR
                    DECKER COAL <0.3 TO O.if PERCENT) TO MEET.S02 EMISSION REGULATIONS.   THE SCRUBBERS WILL  CONTINUE TO OPERATE  IN
                    THE PARTICULATE REMOVAL MODE.
SEP. 76             THE INTERNAL SQ2 SCRUBBING DEMONSTRATION PROGRAM COMMENCED ON OCTOBER  m.   THE SCRUBBERS  OPERATED CONTINUOUSLY
OCT. 76             FOR 10 DAYS.  OPERATION WAS INTERRUPTED BY A FORCED SCRUBBER  OUTAGE RESULTING FROM SCALE  AND SOLIDS CARRYOVER
                    FROM THE WASH TRAY AND MIST ELIMINATOR TO THE SCRUBBER I.D. BOOSTER FAN ASSEMBLY, CAUSING VIBRATION AND
                    BALANCE PROBLEMS.  IT WAS DECIDED TO SANDBLAST THE FAN TO REMOVE SOLIDS BUILDUP ON THE FAN  ASSEMBLY.
                    THE. UTILITY PLANS TO MODIFY THE  COMPONENT'S WASH SYSTEM FOR GREATER FLOW CAPABILITY  AFTER COMPLETION
                                                               26b
                                                                                           PEDCo   ENVIRONMENTAL
                                                                                                  CINCINNATI. OHIO

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                                                FGO SYSTEM PERFORMANCE (CONTINUED)

                                                         ST. CLA1R NO. 6

                    OF THE S02 SCRUBBING PROGRAM.  DECO ALSO PLANS TO CONTINUE PARTICIPATE SCRUBBING FOLLOWING THE

                    TERMINATION OF THE S02 PROGRAM BY UNCOUPLING THE SPRAT TOWERS AND MAINTAINING THE PEABODY-LURGI

                    VENTURI SCRUBBERS IN THE FLUE GAS STREAM. SGML LIMESTONE MAY HAVE TO BE ADDED TO THE PARTICULATE SCRUBBING

                    SOLUTION IN ORDER TO PREVENT LOW PH SWINGS AND MINIMIZE THE POSSIBILITY OF ACID CORROSION DAMAGE TO THE

                    INTERNAL COMPONENTS.

NOV. 76             FOLLOWING THE COMPLETION OF SAND BLASTING OPERATIONS TO SCRUBBER'S I.D. BOOSTER FAN FOR REMOVAL OF SOLIDS

                    BUILD UP, OPERATIONS RESUMED ON NOVEMBER 7 ANU CONTINUED THROUGHOUT  THE MONTH. THE SYSTEM*S  AVAILABILITY

                    INDEX FOR THE MONTH WAS BO PERCENT. THE MAJORITY  OF THE OUTAGE  TIME  WAS CONSUMED PROCURING SAND BLASTING

                    SERVICES.   THE  OPERATION  ITSELF REQUIRED ONLY  8 HOURS.

DEC. 76             THE  S02  DEMONSTRATION  PROGRAM  CONTINUED  THROUGHOUT DECEMBER.  THE SYSTEMS*S AVAILABILITY  INDEX  FOR  THE  PERIOD

                    WAS  si  PERCENT. SCRUBBER  OUTAGES  RESULTED  FROM MALFUNCTIONS OF  THE  LIMESTONE FEEDER*  THE  DENSE SLURRY  TRAVERSE

                    PUMP, THE DENSE SLURRY TANK AGITATORS,  AND PLUGGING  OF THE PH SAMPLE LINE.

JAN.  77             THE  S02 DEMONSTRATION PROGRAM WAS OFFICIALLY TERMINATED ON DEC. 31,  1976. THE SCRUBBER PLANT WAS  SHUT  DOWN  AT

FEB.  77              THIS POINT AND FLUE GAS WAS BY-PASSED AROUND THE  SYSTEM.  THE BOILER REMAINS IN SERVICE,  FIRING LOW SULFUR

 MAR.  77              (0.3X) WESTERN COAL.  CURRENT PLANS CALL FOR  THE  SCRUBBER PLANT TO REMAIN OUT OF SERVICE  UNTIL HID-JUNE  FOR

                     DESIGN AND OPERATIONS MODIFICATIONS. RESUMPTION OF SCRUBBER OPERATIONS WILL OCCUR  IN THE  PRIMARY  PARTICULATE-

                     REMOVAL MODE. THE PEABODY-LUKGI VENTUKI SCRUBBERS AND SPRAY TOWER ABSORBERS WILL REMAIN IN  THE GAS STREAM.

                     SOLUTION WILL BE CIRCULATED THROUGH THE VENTURI«s,  WASH TRAYS,  AND MIST ELIMINATORS.  NO SOLUTION  WILL  BE

                     CIRCULATED THROUGH THE SPRAY ZONE OF THE ABSORBER TOWERS. LIMESTONE REAGENT WILL BE  ADDED TO THE  SCRUBBING

                     SOLUTION IN ORDER TO PREVENT LOW PH SWINGS    AND SUBSEQUENT MATERIALS DAMAGE TO THE SCRUBBER'S INTERNALS.

                     S02 REMOVAL SHOULD RESIDE IN THE 3J> TO SOX   RANGE  IN THIS MODE OF  OPERATION BECAUSE OF THE  SOLUTION'S

                     ALKALINITY DUE TO THE FLY ASH AND LIMESTONE. ALSO.  DECO PLANS TO MAINTAIN A HIGHER L/G RATIO IN THE  SCRUBBER

                     MODULES. THIS MODE Oh OPERATION IS PKOJLCTED TO CONTINUE  FOR A  ONE  TO THREE-YEAR PERIOD FOLLOWING  THE  MID-JUNE

                     RESTART.
                                                                267
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TERMINATED
                 TABLE 16
                SYSTEMS
Ofa/77
IDENTIFICATION NO.


UTILITY NAME


UNIT N*"E


UNIT LOCATION


UNIT RATING


FUEL CHARACTERISTICS


F6D VENDOR


PROCESS


NEW OR RETROFIT


START UP DATE


FGD STATUS


EFFICIENCYt
 PARTICULATES
                    GULF POWER CO.

                    SCHOLZ NO. 1A

                    CHATTAHOOCHEE FLORIDA

                      20 nw

                    COAL   3.0 PERCENT SULFUR

                    AOL/COMBUSTION EQUIP ASSOCIATE

                    DOUBLE ALKALI SCRUBBING

                    RETROFIT

                      2/75
                     99.7  PERCENT
 SOZ



WATER HAKE UP



SLUDGE DISPOSAL
                     95 PERCENT
                     CLOSED LOOP
                     UNSTABILIZED SLUpGE OlSPOSLD IN LINED POND
UNIT COST
OPERATIONAL
 EXPERIENCE
                     REFER  TO THE BACKGROUND INFORMATION SECTION  IN  TABLE  it  OF  THIS  REPORT.
                     THIS PROTOTYPE SCRUBBING SYSTEM WAS INITIALLY PLACED  IN  SERVICE  FEBRUARY
                     1975 AND WAS OPERATIONAL A TOTAL OF H7HH  HOURS  THROUGHOUT THE  YEAR.   THE
                     SYSTEM REMAINED IN SERVICE DURING THE  FOLLOWING 6  MONTHS IN 1976.
                     SUCCESSFUL  COMPLETION  OF THIS PROGRAM  OCCURRED  ON  JULY 2. 1976.  PRESENT
                     PLANS  CALL  FOR A FULL  SCALE EPA-SPONSORED DEMONSTRATION  PROGRAM  WITH
                     THE INSTALLATION SITE  BEING LOUISVILLE GAS & ELECTRIC'S  CANE RUN STATION
                                                           266
                                                                                       PEDCo  ENVIRONMENTAL

                                                                                              CINCINNATI, OHIO 45246

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     THE SCHOLZ STEAM POWER PLANT OF 6ULF POWER COMPANY IS LOCATED IN CHATTAHOOCHEEt FLORIDA.  UNIT NO. 1 IS A COAL-FIRED STEAM
BOILER DESIGNED AND INSTALLED BY BABCOCK AND WILCOX IN 1953.  THIS UNIT IS NOMINALLY RATED AT 40 MW AND IS CAPABLE OF H7.5 MW
MAXIMUM CAPACITY.  THIS UNIT FIRES VARIOUS TYPES OF COAL FOR TEST PURPOSES.  THE AVERAGE CHARACTERISTICS OF THE COAL BURNED IN
THIS UNIT DURING THE FGD DEMONSTRATION PROGRAM ARE*  HEAT CONTENT OF 12,400 BTU/LB* MAXIMUM SULFUR CONTENT OF 5 PERCENT* ASH
CONTENT OF It PERCENT* AND A MAXIMUM CHLORIDE CONTENT OF 0.15 PERCENT.
     A 20-MW PROTOTYPE DUAL ALKALI SYSTEM WAS JOINTLY DEVELOPED, DESIGNED. AND INSTALLED BY COMBUSTION EQUIPMENT ASSOCIATES AND
ARTHUR D. LITTLE.  THE PROTOTYPE SYSTEM AT THE SCHOLZ STEAM PLANT IS INSTALLED ON THE NO. 1 BOILER.  THE SYSTEM IS DESIGNED TO
HANDLE APPROXIMATELY 50 PERCENT OF THE FLUE GAS FROM THE BOILER.  THE BOILER HAS BEEN RETROFITTED WITH A SECTlONALIZED, HIGH-EFF-
ICIENCY ESP  INSTALLED UPSTREAM OF THE FGD SYSTEM AND CAPABLE OF 99.7 PERCENT PARTICULATE REMOVAL.  THE ESP CAN BE SELECTIVELY
DE-ENERGIZED FOR  STUDY  OF  PARTICULATE  IMPACT ON THE FGD OPERATION.
      THE  PROTOTYPE UNIT INCORPORATES A  HIGH DEGREE OF  FLEXIBILITY FOR GENERATION OF  DESIGN  AND  OPERATING  INFORMATION FOR A WIDE
VARIETY  OF  APPLICATIONS.   ALTHOUGH  THE BASIC MODE  OF  SYSTEM OPERATION  is  DUAL  ALKALI WITH LIME  REGENERATION.  THE SYSTEM WAS DE-
SIGNED TO ACCOMMODATE LIMESTONE REGENERATION AND  LIME/LIMESTONE REGENERATION.   THE  SYSTEM CONSISTS  OF  A  VENTURI SCRUBBER AND  AN
ABSORPTION TOWER, WITH AN ADDITIONAL STORAGE SILO FOR LIMESTONE,  A  MIX  TANK,  AND  OTHER  ASSORTED TANKS, PUMPS,  CONTROLLERS, PIPING,
AND A LINED DISPOSAL POND.
      THE PROTOTYPE SYSTEM WAS COMPLETED AND PUT IN OPERATION BY CE.A/ADL IN EARLY  FEBRUARY  1975.  IN MID-MAY  AN EpA  DUAL ALKALI
 TEST PROGRAM WAS INITIATED BY SOUTHERN SERVICES,  CEA» AND AOL.  THE SYSTEM WAS OPERATIONAL  THROUGH  EARLY  JANUARY 1976, WHEN THE
 BOILER WAS  SHUT DOWN FOR A SCHEDULED OVERHAUL.  THE BOILER AND PROTOTYPE  SYSTEM WERE PLACED BACK IN SERVICE  IN EARLY MARCH 1976.
 THE SYSTEM  HAS OPERATED CONTINUOSLY DURING THIS PERIOD ON A HIGH SULFUR COAL (3.5  TO i»,5 PERCENT)  APPLICATION. TREATING FLUE  GAS
 WITH SULFUR DIOXIDE CONCENTRATIONS IN THE. 2000 TO 2500 PPM RANGE.   IN ADDITION,  SYSTEM  WAS  TESTED  OUT  ON  FLUE GAS OF VARYING
 PARTICULATE LOADING TO DETERMINE THE IMPACT OF FLY ASH OF SYSTEM OPERATIONS.   THE  PROTOTYPE PROGRAM WAS  SUCCESSFULLY CONCLUDED
 ON JULY  3,  1976 AT 6 A.M.  RESULTS OF THE PROGRAM ARE BEING PREPARED FUN  PUBLICATION.  THIS PROCESS IS NOW SCHEDULED FOR FULL
 SCALE DEMONSTRATION APPLICATION AT LOUISVILLE GAS AND ELECTRIC*S  CANE  RUN NO.  6 UNIT.
      THE PERFORMANCE OF THE SCHOLZ PROTOTYPE UNIT AND COMMENTS ARE  LISTED BELOW  IN  THE  PERFORMANCE  TABLE.  A  PROCESS FLOW DIAGRAM
 OF THE SCHOLZ PROTOTYPE FGD UNIT IS PROVIDED IN APPENDIX  B.
                                                                265
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                                                     SCHOL2 1A - DOUBLE ALKALI

                     UNIT OPERATING HOURS

          TOTAL                           FGD SYSTEM  PERFORMANCE <*)
  PERIOD  HOURS    BOILER   FGD SYSTEM   OPERABILITY   UTILIZATION                             COMMENTS

 FEB. 75   672       "»59        »»5«»           99           68         UNIT WAS PLACED IN OPERATION FEB. 6, 1975 AND OPERATED UNTIL

 HAR. 75   THH       507        «»85           96           665        JULY 18 WHEN IT WAS SHUT DOWN FOR 2 MONTHS MODIFICATIONSi RE-

 APR. 75   720       60<»        336           56            H7        PAIRS* AND REPLACEMENT OF PARTS.  THE SYSTEM WAS UNAVAILABLE

 HAY  75   7*H       598        375           63            50        TO THE BOILER FOR A <»91-HR PERIOD BECAUSE OF ADJUSTMENTS AND

 JUN. 75   720       720        720           100          100        MODIFICATIONS REQUIRED FOR THE FORMAL EPA TEST  PROGRAM IN

 JUL. 75   7<»«»       683        221           32            30        MID-MAY.

 AUG. 75   7«»«»       7«M»           0          0              0        THE SYSTEM WAS SHUT DOWN FORM MID-JULY TO MID-SEPTEMBER  FOR

                                                                     MECHANICAL OVERHAUL INVOLVING REPLACEMENT PARTS FOR  VALVES

                                                                     THAT HAD FAILED.

 SEP. 75   720       577        25*           «Mt            35        THE SYSTEM WAS PUT BACK IN OPERATION ON SEP 16. 1975.  FROM

 OCT. 75   7«»«*       559        559          100            75        MIO-SEP. TO MID OCT. THE AIR PREHEATER WAS REPAIRED  AND  BOIL-

                                                                     £K OPERATION ADJUSTED To REDUCE OXYGEN LEVELS IN THE FLUE GAS

                                                                     TO THE 5 TO 6 PERCENT RANGE,  THE SYSTEM OPERATED  APPROXI*

                                                                     MATELY 000 MRS. DURING THIS PERIOD.

 NOV. 75   720       620        560           90            78        THE SYSTEM RAN CONTINUOUSLY FOR THE REMAINDER OF THE TEST

 DEC. 75   7H«»       732        732           100           98        PERIOD THROUGH JANUARY 2i  19769  S02 LEVELS DURING THIS  PER-

                                                                     IOD RANGED FROM 800 TO 1700 PPM.  THE SYSTEM OPERATED  IN THE

                                                                     CONCENTRATED MODE THROUGHOUT THE REMAINDER OF THE  TEST PER-

                                                                     IOD.   IN THE PERIOD FROM MID-SPE. TO JAN. 2, i976t THE SYSTEM

                                                                     OPERATED ABOUT 2100 HRS.i  WITH AN OPERABILITY FACTOR OF  97

                                                                     PERCENT.

JAN. 76   7«M»                                                        THE FGD SYSTEM AND BOILER  UNDERWENT A SCHEDULED OVERHAUL OUR.

FEB. 76   696                                                        ING THE REPORT PERIOD.  SYSTEM RESTART IS SCHEDULED  FOR  MID-

                                                                     MARCH  1976. TO CONTINUE UNTIL JUNE.  DURING THIS OPERATING


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                                               SCHOLZ 1A - DOUBLE ALKALI  (CONTINUED)

                     UNIT OPERATING HOURS

          TOTAL                           FGD SYSTEM  PERFORMANCE (X)
  PERIOD  HOURS    BOILER   FGD SYSTEM   OPERABILITY   UTILIZATION                             COMMENTS

                                                                     PERIOD HIGH-SULFUR COAL  13.5-4.0 xj WILL BE BURNED TO ALLOW

                                                                     EVALUATION OF SYSTEM PERFORMANCE ON HIGH-SULFUR COAL.

MAR. 76   744       7*2       445            60            60        THE  SYSTEM WAS PUT BACK  IN SERVICE ON MAR. 12, 1976.  THE TO-

                                                                     TAL  NUMBER OF OPERATING  HRS. FOR THE MONTH OF MAR. MAS 445

                                                                     HRS.  THIS TRANSLATES  INTO A 94X OPERABILITY FACTOR SINCE THE

                                                                     MAR. 12  RESTART.

APR. 76   720       642         616           96            86        SOME MINOR MECHANICAL  PROBLEMS IN  THE FORM OF AGITATOR SHAFT

MAY 76   744       735         651           89            68        AND CONTROL  VALVE FAILURES WERE ENCOUNTERED  DURING THE REPORT

                                                                     PERIOD.   SINCE THE SYSTEM RESTART  ON MAR.  12, HIGH-SULFUR

                                                                     COAL HAS BEEN BURNED IN THE  BOILER (3.5 TO 4.5 X  SULFUR), RE-

                                                                      SULTING IN THE S02 INLET CONCENTRATION  LEVELS  IN THE  2000 TO

                                                                      2&00 PPM RANGE.

 JUN. 76   720       656        641           93            89        DURING THE LAST PHASE OF OPERATION,  THE SYSTEM WAS TREATING

                                                                      FLUE GAS OF VAkYING PARTICIPATE LOADS.   THE  UPSTREAM  ESP WAS

                                                                      WAS SELECTIVELY DE-LNERGIZEO,  BOTH PARTIALLY AND  TOTALLY.  NO

                                                                      MAJOR USETS IN THE PROCESS CHEMISTRY OCCURRED.   BOILER LOAD

                                                                      VARIATION RANGED FROM 30 TO  100*.   THE  PROTOTYPE  PROGRAM AT

                                                                      THE PLANT WAS SUCCESSFULLY CONDUCTED ON JULY 2.   AOL  is  CURR-

                                                                     ENTLY COMPLETING DATA ACQUISITION  AND  ANALYSIS.

 JUL. 76   744        54*        54          100*                    THE PROTOTYPE TEST PROGRAM WAS SUCCESSFULLY  CONCLUDED ON JULY

                                                                     3* 1976.

                                                                     •NOTE*  THE  BOILER HRS.,  SYSTEM OP  HRS., AND  THE CORRESPONDING

                                                                             PERFORMANCE VALUE CALCULATED  INCLUDES SYSTEM OP UP TO

                                                                             THE  SCHEDULED SHUTDOWN, ON  JULY  3, 6*00 A.M.,  1976.


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                 TABLE  it.
 TERMINATED F60 SYSTEMS
         Ob/77
IDENTIFICATION NO.
UTILITY NAME
UNIT NAME
UNIT LOCATION
UNIT RATING
FUEL CHARACTERISTICS
FGD VENDOR
PROCESS
NEW OK RETROFIT
START UP DATE
FGD STATUS
EFFICIENCY,
 PARTICULATES

 S02

WATER MAKE UP

SLUDGE DISPOSAL
UNIT COST
OPERATIONAL
 EXPERIENCE
GULF POWER CO.
SCHOLZ NO. 2 A
CHATTAHOOCHEE FLORIDA
  20 MW
COAL   3.0 PERCENT SULFUR
FOSTER WHEELER
ACTIVATED CARBON
RETROFIT
 2/76


99.7 PERCENT

7H.5 PERCENT  (DESIGN)

N/A DRY  ADSORPTION SYSTEM
REFER TO THE BACKGROUND INFORMATION SECTION IN TABLE 16 OF THIS
REPORT.  THIS IS A PROTOTYPE DRY ADSORPTION REGENERABLE SYSTEM
DESIGNED BY FOSTER WHEELER AND BER&BAU FORSCHUNG.  OPERATION OF
THE PROTOTYPE UNIT DURING THE SCHOLZ DEMONSTRATION PROGRAM PROCEEDED
ON AN INTERMITTENT BASIS.  OPERATIONAL SEGMENTS OCCURED IN AUGUST 1975,
OCTOBER 1975. AND MARCH, APRIL AND MAY 1976.  SYSTEI OPERATIONS HERL
PREMATURELY TERMINATED AT THIS POINT AND THE PHOTOTYPE UNIT WAS SHUT
DOWN.  THE SYSTEM IS CURRENTLY INACTIVE.
                                                           272
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     IN JANUARY 1973. THE SOUTHERN SERVICES COMPANY OF GULF POWER AWARDED  A  CONTRACT  TO  THE FOSTER  WHEELER CORPORATION TO BUILD A

20-MW PROTOTYPE DRY ADSORPTION SYSTEM FOH FLUE GAS DESULFURIZATIUN.  CONSTRUCTION  ON  THE FOSTER  WHEELER  PROCESS STARTED FEBRUARY

15t 1971*. AT THE SCHOLZ STEAM POWER PLANT IN CHATTACHOOCHEE» FLA.  CONSTRUCTION  WAS COMPLETED AND A TESTING PROGRAM WAS INITIATED

IN MAY 1975.

     THE SYSTEM AT THE SCHOLZ PLANT CONSISTS OF  A 20-Mb,  ADSOKBER SECTION AND A «»7.5-MW REGENERATION AND  REDUCTION SECTION.  THE 20

HW ADSORBER IS DESIGNED TO ACCEPT HALF OF THE MAXIMUM FLUE GAS  FLOW  FROM UNIT NO.  2.   THE COAL-FIRED BOILER IS RATED AT 40 MW

I NOMINALI»  IT FIRES COAL WITH AN AVERAGE HEATING VALUE 0*  12.HOO bTU/Lb.   MAXIMUM  ASh AND SULFUR CONTENTS ARE 1» AND 3 PERCENT,

RESPECTIVELY.

      THE PURPOSE  OF  THE  ADSORPTION  SECTION  OF  THE  FWBF  uRY REMOVAL  SYSTEM IS TO  REMOVE SULFUH UlUXIDEi NITROGEN OXIDES. AND

PARTICULATE FROM  THE  FLUE  GAS  WITH  ACTIVATED CHAR,  CONVERTING THE  CAPTURED POLLUTANTS TO SULFURIC ACID.  THE REGENERATION SECTION

PROVIDES CONTINUOUS ON-SITE REGENEhATION OF THE CHAR. WHICH HAS BLEN LOADED WITH SULFUR DIOXIUE  IN THE FORM OF SULFURIC ACID.  THE

 CHAR IS REGENERATED AMD A LOw-VOLUME, SULFUR DIOXIDE-HICH OFF-GAS STREAM  IS FEU FORWARD TO  THL RESOX REACTOR, WHICH REDUCES THE

 SULFUR DIOXIDE STREAM TO GASEOUS ELEMENTAL SULFUR THAT  IS COLLECTEU AND STORED  IN AN  INSULATED TftNK.

      THE DEMONSTRATION UNIT HAS TWO ROkS OF MODULES, EACH R0«  CONSISTING  UF  SIX MODULES.   THE ADSORPTION  SECTION  IS A  TWO-STAGE

 DESIGN CONSISTING OF VERTICAL COLJFNS OF PAHALLEL LOUVEK BLDS  WH1LH SUPPOKT  ANU CONTAIN THt ftCTIVATEO CHARCOAL.   SULFUR DIOXIDE,

 OXYGEN, WATER VAPOR, AND NITROGEN OXIDES ARE ADSORBEL BY THE CHAK PELLETS FROM  THE CROSS.FLOWING FLUE GAS  AT 250  TO 300 F.  THE

 SULFUR DIOXIDE THEN REACTS WITH OXYGEN A"0 WATER TO FOKM SULFURIC ACID WHICH IS FIRMLY  RETAINED  IN  THE  INTERIOR PORE  SYSTEM OF

 THE  CHAR PELLETS.  THE CHAR IS THEN REGENERATED IN THE  REGENERATOR  VESSEL BY HEATING  TO 1200 F,  DRIVING  OFF THE ENTRAINED GASES,

 AND  REDUCING SULFURIC ACID TO SULFUR DIOXIDE.   THE SULFUR DIOXIDE-RICH GAS  IS THEN PASSED  THROUGH  A  VESSEL CONTAINING  CRUSHED

 COAL,  RESULTING  IN REDUCTION TO GASEOUS ELEMENTAL SULFUR ftMD CARBON DIOXIDE.  THIS LATTER  PROCESS  IS CARRIED OUT  AT J200  TO

 isoo F.  A SCHEMATIC OF THE PROCESS COMPONENTS  FOR THE  FW-BF DKY ADSORPTION  is PRESENTED IN APPENDIX B.

       THE INITIAL SHAKEDObN ON FLUE GAS BEGAN AUG. 11, 1975, ANU PROCEEDED CONTINUOUSLY  FOR  10 OAyS.  THE  REGENERATION  SECTION WAS

 OPERATIONAL ABOUT 60 PERCENT OF THE TIME.  HOWEVER, THE REDUCTION SECTION HAS NOT YET BEEN  INTEGRATED INTO SYSTEM OPERATION.  SUL-

 FUR  DIOXIDE REMOVAL WAS WELL ABOVE EXPECTATIONS AND PRESSURE DROP ACROSS  THE ADSORBER WAS  WELL BELOW DESIGN LEVELS.   THE  SYSTEM

 WAS  SHUT DOWN FOR CORRECTION OF SEVERAL OPERATING PROBLEMS, EQUIPMENT MODIFICATIONS.  AND EVALUATION  OF THE INITIAL OPERATING

 DATA.  OPERATION WAS RESUMED IN OCTOBER 1975. WHEK Tk'O  CONSECUTIVE RUMS WERE CONDUCTED  WITH THE  REDUCTION  PORTION OF  THE  SYSTEM

 PROCESSING FRONT-END OFF-GAS AT FULL OPEKATING  TEWPEKATUKES.   A PROGRAM OF MODIFICATION WAS COMPLETED ON  THIS SYSTEM  IN EARLY
                                                                273
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                                              SCHULZ NO.  2A  -  FWBF  SYSTEM  (CONTINUED!

JANUARY 1976.   REINTROOUCTION OF FLUE GAS  INTO THE  INTEGRATED  SYSTEM  COMMENCED  IN  FEBRUARY  1976.   OPERATIONS  THROUGH  A  FINAL

H-HONTH TEST PROGRAM  WERE PREMATURELY TERMINATED  ON MAY 2.  1976.
                                                               27>»
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                                                  FHBF SYSTEM OPERATING HISTORY

PERIOD                                                      COMMENTS

HAT  75            COMPLETION OF CONSTRUCTION WAS FOLLOWED BY A 3-MONTH COMMISSIONING PERIOD DURING WHICH

JUN. 75            VARIOUS PIECES OF EQUIPMENT WERE OPERATED INDIVIDUALLY AND THEN IN COMBINATIONS To

JUL. 75            SIMULATE SUBSYSTEM OPERATION.  SUBSYSTEM OPERATIONS HERE INTEGRATED INTO SECTION

AUG. 75            OPERATIONS AND FLUE GAS WAS PASSED THROUGH THE ADSORBER AND REGENERATOR FOR A 10-UAY

                   PERIOD BEGINNING AUGUST 11.  RESOX CONSTRUCTION WAS INCOMPLETE AT THIS TIME.

OCT. 75            TWO CONSECUTIVE RUNS WERE CONDUCTED ON THE RESOX PORTION OF THE SYSTEM ON FRONT.END

                   PROCESS OFF-GAS AT FULL OPERATING TEMPERATURES.  THIS OPERATIONAL PERIOD LASTED 5 DAYS.

NOV. 75            A PROGRAM OF MODIFICATIONS ON THE SYSTEM BEGAN IN LATE AUGUST 1975 AND CONTINUED

DEC. 75            THROUGH JAN. 1976. WITH THE EXCEPTION OF THE 5-DAY RESOX OPERATION IN OCTOBER.

JAN. 76            MODIFICATIONS WERE COMPLETED AND PRE-STARTUP TESTING WAS CONDUCTED IN LATE JANUARY

                   AND EARLY FEBRUARY.  A 3-DAY CONTINUOUS DRY RUN WAS SUCCESSFULLY COMPLETED.

FEB. 76            ALL MATERIALS-HANDLING LOOPS AND HESOX LOOPS WERE OPERATED AT FULL OPERATING

                   TEMPERATURES AND PRESSURES.  REENTRODUCTION OF FLUE GAS INTO THE SYSTEM COMMENCED,

                   AND A 4-HONTH FORMAL TEST PROGRAM CONDUCTED BY SOUTHERN SERVICES AND FOSTER WHEELER

                   IS NOW IN PROGRESS.

MAR. 76            THREE OPERATIONAL PERIOuS WERE LOGGED BY THE PROTOTYPE SYSTEM DURING THE REPORT

PAR. 76            MONTHS.  DURING THESE RUNS THE ADSORPTION AND REGENERATION SECTIONS PERFORMED

                   ADEQUATELY.  THE RESOX SECTION OPERATED INTERMITTENTLY BECAUSE OF PLUGGING PROBLEMS

                   IN THE SULFUR CONDENSER.  ALSO. THE FRONT END OF THE SYSTEM WAS TAKEN DOWN AT ONE

                   POINT DUE TO FREQUENT HIGH TEMPERATURE EXCURSIONS.  THIS PROBLEM WAS CORRECTED BY

                   MODIFYING SYSTEM OPERATING PROCEDURES.  CURRENTLY, WORK IS PROCEEDING ON THE

                   SOLUTION OF THE SULFUR CONDENSER PROBLEM.

MAY  76            THF FW-BF UNIT COMPLETED AN OPERATIONAL PERIOD IN EARLY MAY WHICH HAD COMMENCED ON

                   APRIL 26.  THE SYSTEM WAS TAKEN DOWN AT THIS POINT FOR THE FOLLOWING REASONS*
                                                               275               f^
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                         FhHF STSTtM OPERATING HISTORY ICONTINUEUI

                                        COMMENTS

*    DEPLETION OF CHAK SUPPLY.

*    HIGH CHAR CONSUMPTION  RATES DUE TO MECHANICAL  ATTRITION.

*    CORRECT/MODIFY THE CHAR/SAND SCREEN SEPARATOR.

AT THIS POINT THL DECISION  WAS  MAUL TO  PREMATURELY  TERMINATE THE FW-BF DEMONSTRATION

PROGRAM RATHER THAN SHUT OOWNt  DEBUG.  AND RESTART THL  SYSTEM AGAIN.  THt SYSTEM

SUPPLIER IS PURSUING ADDITIONAL FUNDING FOR  THE CONTINUATION OF THE PROTOTYPE

DEMONSTRATION PROGRAM.
                                                                        PEDCo  ENVIRONMENTAL
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                 TABLE 16
 TERM IN ATE. 0 FGO SYSTEMS
          06/77
IDENTIFICATION NO.


UTILITY NAME


UNIT NAME


UNIT LOCATION


UNIT RATING


FUEL CHARACTERISTICS


FGD VENDOR


PROCESS


NEW OR RETROFIT


START UP DATE


FGO STATUS


EFFICIENCY!
 PARTICULATES
 GULF f-OWER CO.


 SCHOLZ NOS. IB X 2B


 CHATTAHOOCHEC FLORIDA


   23 MW


 COAL 5.0 PERCENT SULFUR (MAX)


 CHIYODA INTERNATIONAL


 THOROUGHBRED 101


 RETROFIT


  3/7b






 99.7 PERCENT
 S02
WATER HAKE UP
SLUDGE DISPOSAL
UNIT COST
OPERATIONAL
 EXPERIENCE
 90 PERCENT
 OPEN LOOP
 UNSTABILIZEQ SLUDGE DISPOSED IN DRY GYPSUM POND
S3 MILLION CAPITAL COST
 REFER TO THE BACKGROUND INFORMATION IN TABL E I&OF THIS REPORT.  CHIYOOA
 AND GULF POWER ANNOUNCED ON MAHC THE COMPLETION OF Thl& DEMONSTRATION
 PROGRAM.  DURING JANUARYt FEBRUARYt AND MARCH OPERATIONS, THERE WERE ONLY
 20 MINUTES OF FORCED SCRUBBER OUTAGE.  UTILIZATION WAS ESSENTIALLY 100
 PERCENT UNTIL PROGRAM TERMINATION.  PROCESS UTILIZATION WAS GREATER THAN
 99 PERCENT FROM OCT. 17 THROUGH PROGRAM COMPLETION.  SOUTHERN SERVICES
 IS CURRENTLY PKEPAKlNG A COMPREHENSIVE REPOKT ON THE CT-101 FGD SYSTEM
 DEMONSTRATION PROGRAM AT GULF POWER.
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                                                      BACKGROUND INFORMATION

                                                                ON

                                                  SCHOLZ UNITS 1 AND 2 - CHIYODA

     THE SCHOLZ POWER PLANT IS LOCATED IN CHATTAHOOCHEE. FLORIDA. ABOUT 50 MILES WEST OF TALLAHASSEE.  THE FSO SYSTEM WAS DESIGNED

BY CHIYOOA INTERNATIONAL CORP. FOR TESTING AND PROCESS DEMONSTRATION ON A COAL-FIRED APPLICATION.  THE PROCESS IS USED IN JAPAN

EXCLUSIVELY ON OIL-FIRED AND GAS-FIRED BOILERS, AND TAIL GAS FKOM CLAUS UNITS.

     THE SYSTEM AT SCHOLZ CAN HANDLE ONE-HALF THE LOAD (S3.000 SCFHI FROM EITHER OF THE <*0-MW NOMINALLY RATED BOILERS. WHICH WERE

DESIGNED AND INSTALLED BY BABCQCK AND WILCQX IN 1953.  DLSIGN ABSuRBER INLET SULFUR DlQXIUE CONCENTRATION IS 2250 PPM.  VARIOUS

TEST COALS WITH SULFUR CONTENTS RANGING UP TO 5 PERCENT ARE SCHEDULED FOR BURNING.

     THE PARTIcULATE LOADS FROM NEWLY INSTALLED ELECTROSTATIC PREcIPITATORS ON THE TWO UNITS RANGE FROM 0.02 TO 0.1 GR/ScF.  FLUE

GAS FROM THE PRECIHITATORS IS SlUENCHLD WITH COOLING WATER TO REMOVE ADDITIONAL FLY ASH AND TO COOL THE GAS BEFORE IT ENTERS THE

SULFUR DIOXIDE ABSORBER.

     SULFUR DIOXIDE IS ABSORBED IN WATER AND CATALYTICALLY OXIDIZED WITH AIR TO FORM SULFURIC ACID.  THE DILUTE ACID IS RECIRCU-

LATED THROUGH THE ABSORBER.  A PORTION OF THE ACID is NEUTRALIZED WITH LIMESTONE TO PRODUCE GYPSUM AS A BY-PRODUCT.

     BREAK.IN TESTING COMMENCED IN FEBRUARY 1975. THE FIRST FEW MONTHS OF THE SHAKEDOWN PERIOD WERE CHARACTERIZED BY MANY MINOR

PROBLEMS, RESULTING IN A LOW OPERABILITY INDEX VALUE <3o* FOR FEU-MAY). MANY OF THESE PROHLEMS W^RE RESOLVED BY JUNE. (MANIFESTED

BY A HIGHER OPERABILITY INDEX <8<»X> VALUE FOR THE JUNE-JULY PERIOD). A 6-WEEK SCRUBBER OUTAGE PERIOD COMMENCED IN AUGUST FROM

UNBALANCING OF THE GYPSUM CENTRIFUGES.  AFTER REPAIR OF THE CENTRIFUGES AND INSTALLATION ON SEPTEMBER 15, THE OPERABILITY INDEX

THROUGH DECEMBER 1975, AVERAGED ABOVE 97 PERCENT.

     CHIYODA. GULF POWER, AND SOUTHERN COMPANY SERVICES SUCCESSFULLY CONCLUDED CT-101 OPERATIONS ON MARCH 22. 1977, AFTER MORE

THAN TWO YEARS OF INTENSIVE TESTING, EVALUATION, AND DEMONSTRATION. INFORMATION AND UATA CONCERNING THE OPERATION OF THE

Ct-101 PROTOTYPE UNIT A«E PRESENTED IN THE PERFORMANCE TABLE THAT FOLLOWS.  A PROCESS FLOW DIAGRAM IS IN FIGURE 6, APPENDIX C.
                                                               270
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                                                   SCHOL2 IB AND 28 - CHIYOOA
MONTH

FEB. 75



APR. 75

HAY  75
TOTAL
HOURS

  672
  720

  744
JUN. 75    720

JUL. 75    744
AU6. 75    744

SEP. 75    720
OCT. 75    744
NOV. 75    720
  UNIT OPERATING HOURS

BOILER    FGD SYSTEM

   672
             FGO SYSTEM PERFORMANCE (X)
           OPERABILITY    UTILIZATION
   720

   744
200

100
20

13
26

13
             685

             744
             720
              665

              624
                0

              337
                100

                 8*
               95

               84
                                                                 46
             744
             720
              744
              720
                                        100
                100
              000



              100

             279
                       COMMENTS

THIS IS A PILOT PLANT SIZE DEMONSTRATION UNIT.

PRELIMINARY ENGINEERING AND DESIGN WORK BEGAN IN

1973.  INITIAL SHAKEDOWN AND DEBUGGING OPERATIONS

COMMENCED ON FEBRUARY 11, 1975.  PROBLEMS

ENCOUNTERED INCLUDED CRACKS IN THE FRP LINING AT

THE OXIDIZING TOWER.  STARTUP OCCURRED IN MARCH

1975.  AFTLR INITIAL OPERATION FOR BREAK-IN TESTS,

THE UNIT WAS SHUT DOWN FOR INTERNAL INSPECTION.

RELIABILITY TESTS THEN FOLLOWED IN JULY 1975,

CHEMICAL PERFORMANCE WAS SATISFACTORY.  EMISSION

TESTS HAVE NOT BEEN PERFORMED.  SOME PUMP AND

INSTRUMENT FAILURES HAVE OCCURRED.

A 100 PERCENT OPERABILITY FACTOR WAS REGISTERED

FOR THE MONTH OF JUNE.  DURING THE MONTH OF JULY

ONE CENTRIFUGE BECAME UNBALANCED. REQUIRING THE

SPARE TO BE PLACED IN SERVICE.

DURING THE MONTH OF AUGUST BOTH CENTRIFUGES BECAME

UNBALANCED REQUIRING A FORCED OUTAGE WHICH

EXTENDED TO MID-SEPTEMBER.  UNIT OPERATED AT A

95 PERCENT S02 REMOVAL EFFICIENCY DURING THIS

PERIOD.  GULF POWER IS ATTEMPTING TO UPGRADE THIS

VALUE TO A HIGHER EFFICIENCY LEVEL.

WASTE WATER DISCHARGE FRQM THIS UNIT STILL A

PROBLEM AREA.

OUTAGE TIME. WAS LESS THAN ONE HOUR DURING NOVEMBER
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                                                   SCHOLZ IB AND  2B  -  CHIYOOA  (CONTINUED)
                     UNIT OPERATING HOURS
         TOTAL                                FGD SYSTLH PERFORMANCE  (X)
         HOURS     BOILER    FGD SYSTEM     OPERABILITY     UTILIZATION
MONTH
NOV. 75 (CONTINUED)
DEC. 75
JAN. 76
FEB. 76
           696
680
690
                                 726
H50
 77
                                                 98
66
11
                                                                98
60
11
WAR. 76
APR. 76
          720
7f«t
720
7V1
101
                                                100
              100
RAY  76
JUN. 76
                                                               260
                       COMMENTS
OPERATION DUE TO A BROKEN FLUE GAS BLOWER INLET
VANE AND REPAIR OF A PINHOLE IN THE PRESCRUBBER
FRP LINING.
SCRUBBEK OUTAbES DURING DECEMBER RESULTED FROM
CONTINUING REPAIRS TO A PINHOLE IN THE PRESCRUBBER
FRP LINING.
OUTAbE TIME IN JANUARY-FEBRUARY WAS PRIMARILY FOR
REPAIR AND MODIFICATION OF THE SUCTION AND DIS-
CHARGE PIPING ON THE ABSORBENT CIRCULATION PUMPS.
THESE FRP LINES BROKE IN JANUARY AT SOME WEAK
FIELD JOINTS.  S02 REMOVAL EFFICIENCY HAS BEEN AS
HIGH AS 95*.
PLANT WAS STOPPED APRIL 5 FOR A SCHEDULED SHUTDOWN
TO ALLOW INSTALLATION AND MODIFICATIONS FOR
REDUCING THE QUANTITY OF LIQUID WASTE FROM THE
SYSTEM.  START-UP AND TESTING OF THIS MODIFICATION
WAS PLANNED FOR THE FIRST WEEK IN MAY.  A FIRE AT
THE PLANT. HOWEVERt NECESSITATED A DELAY IN
SYSTEM RESTART FOR AN ADDITIONAL 3 TO * WEEKS.
THE SYSTEM WAS SHUT DOWN APRIL 2* BECAUSE OF
EXTENSIVE FIRE DAMAGE IN THE OXIDIZING TOWER.
THE FIRE. CAUSED BY A WELDING ACCIDENT.
DAMAGED FRP AND POLYPROPYLENE COMPONENTS IN
THE OXIDIZING TOWER.  REPAIRS CONTINUED AS
THE SYSTEM REMAINED OUT OF SERVICE DURING

            PEDCo   ENVIRONMENTAL
                   CINCINNATI. OHIO 45246

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                                                 SCHOLZ  IB AND 28 - CHIYOOA  (CONTINUED)
MONTH
JUL. 76

AUG. 76
         TOTAL
         HOURS
  UNIT OPERATING HOURS

BOILER    FGD SYSTEM
  FGO SYSTEM PERFORMANCE  (X)
OPERABILITY    UTILIZATION
              1(92
                                              66
                       COMMENTS

THE REPORT PERIOD.   SYSTEM RESTART  IS

SCHEDULED FOR THE END OF JULY.

T«E PROTOTYPE UNIT REMAINED OUT  OF  SERVICE

MAYt JUNE AND JULY TO REPAIR THE FIRE-DAMAGED

AREAS.  THE SYSTEM WAS PUT BACK  IN  OPERATION

IN AUGUST.  THE SYSTEM WAS AGAIN BROUGHT  DOWN

DURING THE MONTH TO COMPLETE ADDITIONAL REPAIRS

WHICH WENT UNDETECTED DURING THE PREVIOUS

OUTAGE.  241.67 HOURS OF THE 251.75 HOURS

OF AUGUST OUTAGE TIME WAS CONSUMED  FOR THESE

ADDITIONAL REPAIRS.  THE WATER SAVINGS PRO-

GRAM IS NOW BEING CONDUCTED ON THIS SYSTEM.

BASICALLYt THIS TEST PROGRAM CALLS  FOR A

REDUCTION IN WASTEWATER SLOWDOWN AND FRESH

WATER MAKEUP REQUIREMENTS BY RECYCLING THE

MOTHER LIOUOR BLEED BACK TO THE  PROCESS FOR

ADDITIONAL SERVICE.
                                                              261
                                                                         PEDCo  ENVIRONMENTAL-
                                                                                CINCINNATI. OHIO

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                                                 SCHOLZ IB AND «>b - CHIYODA 
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MONTH
TOTAL
HOURS
                                             SCHOLZ 18 AND 2B - CHIVO0A (CONTINUED)
                     UNIT OPERATING HOURS
                                              FGD SYSTEM PERFORMANCE  i»
                   BOILER    F60 SYSTEM  AVAILABILITY  OPERABILITY      RELIABILITY   UTILIZATION
JAN. 77
FEB. 77
MAR. 77
          672
7'K
672
                      672
100
100
100
100
100
100
100
100
100
100
     THE PROGRAM WAS TERMINATED TO ALLOW CIC TO DEVELOP AND DEMONSTRATE A NEW F6D DESIGN.
     NO DEMONSTRATION COMMITMENTS HAVE YET BEEN MADE.
          COMMENTS
PROBLEMS INCLUDED A MALFUNCTION OF
A LEVEL INDICATOR, A BROKEN
GUIDE VANE* AND AN OPERATOR ERROR
RESULTING IN A LEAK OF SLURRY INTO
THE WATER HEADER.  ON NOV.lt SOU-
THERN SERVICES FINISHED ITS ScHOLZ
EVALUATION OF THE CT-101.  A PER-
FORMANCE REPORT IS DUE SPRING 1977.
GULF POWER WILL CONTINUE OPERATION
OF THE CHIYOOA UNIT FOR AN UNSPE-
CIFIED PERIOD IN 1977.
CIC, GPC, 1 SCS SUCCESSFULLY CON-
CLUDED THE CT-101 TESTING AND DE-
MONSTRATION PROGRAM ON MARCH 22.
DURING THE REPORT PERIOD, THE TOTAL
SCRUBBER OUTAGE TIME WAS 0.33 HR.
THE SYSTEM HAS BEEN IN SERVICE ON A
VIRTUALLY CONTINUOUS BASIS SINCE
OCT. 17« TOTALLING OVER 3 MONTHS OF
100* RELIABLE OPERATION.
                                                               283
                                                                                          PEDCo  ENVIRONMENTAL
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                 TABLE 16
 TERMINATED FGO SYSTEMS
          Ob/77
 IDENTIFICATION NO.
 UTILITY NAME
 UNIT NAME
 UNIT LOCATION
 UNIT KATINS
 FUEL CHAKACTERISTICS
 FGO VENDOR
 PROCESS
 NEW OR RETROFIT
 START UP DATE
 FGO STATUS
 EFFICIENCYt
 PARTICIPATES
 ILLINOIS POWER
 WOOD RIVER NO t
 EAST ALTON ILLINOIS
  110 MW
 COAL   2.9-3.2 PERCENT SULFUR
 MONSANTO ENVIRO CHEN SYSTEMS
 CATALYTIC OXIDATION
 RETROFIT
 10/72


 99 PERCENT
 S02
WATER HAKE UP
SLUUGE DISPOSAL
UNIT COST
OPERATIONAL
 EXPERIENCE
 85 PERCENT
•82.5/KW CAPITAL * S952tOOO OPERATING
 REFER TO THE BACKGROUND INFORMATION SECTION IN TABLE 16.  SYSTEM START-UP
 OCCURRED IN OCTOBER 1972.  INITIAL AND SUBSEQUENT OPERATIONS WERE
 ACCOMPANIED BY A NUMBER OF SEVERE MECHANICAL-RELATED PROBLEMS RESULTING
 IN LIMITED OPERATIONS ANU EVENTUAL TERMINATION OF THE PROGRAM.  TOTAL
 OPERATION TIME WAS <»«»H HOURS IN 1972* 156 HOURS IN 1973 AND 55 HOURS IN
                                                           264
                                                                                         PEDCo  ENVIRONMENTAL
                                                                                               CINCINNATI. OHIO

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     THt WOOD RIVER POWER STATION OF THE ILLINOIS POWER COMPANY IS LOCATED NEAR EAST ALTON, ILLINOIS, NORTH OF ST.  LOUIS.  HISS-
OURI.  THE NO. H BOILER IS A COMBUSTION ENGINEERING PULVERIZED-COAL-FIRLD UNIT THAT HAS A GROSS RATED CAPACITY OF 109 MW AND A
NET CAPACITY OF 103 MW,  THIS UNIT FIRES A HIGH SULFUR CENTRAL ILLINOIS COAL WITH TYPICAL CHARACTERISTICS OF 3.1  PERCENT SULFUR,
10 PERCENT ASH AND A HEAT CONTEN*. OF 10,800 BTU/LB.  ANNUAL COAL CONSUMPTION IS APPROXIMATELY 275.000 TONS/YEAR.
     THE EMISSION CONTROL EQUIPMENT FOR THIS BOILER INCLUDES MECHANICAL COLLECTORS. A HIGH EFFICIENCY ESP, AND A  MONSANTO CATALY-
TIC OXIDATION (CATOX) FGD SYSTEM FOR THE CONTROL OF PARTICULATES AND SULFUR DIOXIDE.  DESIGN REMOVAL EFFICIENCIES OF THIS CONTROL
SYSTEM ARE 99.9 PERCENT FOR PARTICULATES AND 65 PERCENT FOR SULFUR DIOXIDE.  INLET SULFUR DIOXIDE CONCENTRATIONS  TO THE CATOX SYS.
TEM ARE GENERALLY IN THE 2000 TO 2200 PPM RANGE.
     FOLLOWING PASSAGE THROUGH THE PARTICULATE REMOVAL SYSTEM, THE FLUE GAS ENTERING THE SCRUBBING SySTEM IS HEATED TO A TEMPERA-
TURE OF 850 F AND PASSES THROUGH A VANADIUM PENTOXIDE FIXED-BED CATALYTIC CONVERTER, WHERE THE SULFUR DIOXIDE IS  OXIDIZED TO
SULFUR TRIOXIDE.  THE GAS THEN FLOWS THROUGH AN ACID ABSORPTION TOWER, WHERE THE SULFUR TRIOXIOE IN THE GAS IS CONVERTED TO SUL-
FUR 1C ACID.  AN ACID MIST ELIMINATOR ENSURES REMOVAL OF ENTRAINED ACID MIST FROM THE GAS STREAM.  THE CLEANED GAS IS DISCHARGED
TO THE STACK AND THE PRODUCT ACID IS COOLED AND STORED IN TANKS.  A SIMPLIFIED PROCESS FLOW DIAGRAM UF THE WOOD RIVER CATOX SYS-
TEM IS PRESENTED IN APPENDIX B.
     THIS DEMONSTRATION SYSTEM, PARTIALLY FINANCED BY EPA, WAS STARTED UP IN SEPTEMBER 1972.  WHILE THE MAIN PARTS OF THE UNIT
PERFORMED ACCEPTABLY, VARIOUS TROUBLES WITH ASSOCIATED EQUIPMENT CAUSED EXTENSIVE SHUTDOWNS AND DELAYS, TO THE EXTENT
THAT APPROXIMATELY 27 DAYS OF FULL OPERATION HAS BEEN OBTAINED IN ALMOST TWO YEARS.  A 24-HOUR PERFORMANCE TEST RUN WAS COMPLETED
IN JULY 1973.  THE FOLLOWING GUARANTEES WERE ACHIEVED AND EXCEEDED*  90 PERCENT CONVERSION OF SULFUR DIOXIDE TO SULFUR TRIOXIDE
(ABOUT 85 PERCENT NET REMOVAL). 99 PERCENT REMOVAL OF PARTICULATE ENTERING THE SYSTEM, LESS THAN 1 MG/ACF OF ACID MIST IN GAS
LEAVING SYSTEM, PRODUCTION OF 60 DEGREES BAUME ACID.
PERFORMANCE SUMMARY
     THE WOOD RIVER SYSTEM WAS STARTED-UP IN SEPTEMBER 1972 BUT WAS SHUT DOWN ALMOST IMMEDIATELY (IN OCTOBER) TO CONVERT THE BURN-
ERS TO OIL FIRING, WHICH WAS NOT COMPLETED UNTIL JUNE 1973.  A SUCCESSFUL PERFORMANCE TEST WAS THEN MADE, BUT BECAUSE OF THE
CATALYST PLUGGING HAZARD THE SYSTEM WAS SHUT DOWN AGAIN TO INSTALL AN EXTERNAL BURNER SYSTEM, WHICH WAS NOT COMPLETED UNTIL APRIL
197*.  VARIOUS OTHER PROBLEMS WITH STANDARD EQUIPMENT HAVE BEEN ENCOUNTERED SINCE. WITH THE RESULT THAT ONLY 657  HOURS OF
OPERATING TIME HAVE BEEN LOGGED IN ALMOST TWO YEARS.
     SEVERAL OTHER MAJOR PROBLEM AREAS ENCOUNTERED DURING THE INTERMITTENT OPERATION OF THIS REGENERABLE SYSTEM INCLUDED*  FROZEN


                                                               265                "   ' xx PEDCo  ENVIRONMENTAL
                                                                                                   CINCINNATI. OHIO 45246

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                                                  WOOD RIVEK NO. <» (CONTINUED)

DAMPERS ON REHEAT  BURNERS. CRACKS IN THE TEFLON LINER ON THE ACID PUMP'S DISCHARGE HEADER.  CRACKS IN THE  REHEAT  DUCTIN6.  FALL  OF

REFRACTORY BRICKS  FRO« THE REHEATER BUHNER DOME, AND NEED FOR REINFORCEMENT OF THE STRUCTURE SUPPORTING THE  HIGH TEMPERATURE FLUE

GAS DUCT TO THE  CATALYTIC CONVERTER.
                                                              286
                                                                                           PEDCo  ENVIRONMENTAL
                                                                                                  CINCINNATI. OHIO

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DATE
10-8-72
10-9-72
10-10-72
10-13-72
10.11-72
10-30-72
10-31-72
7-21-73
7-22-73
7-23-73
7-21-73
7-25-73
7-26-73
7-17-73
7-28-73
7-29-73
HOURS
21
21
18
20
16
21
16
18
21
18
21
11
13
19
19
9
                                                   of*f.n*rxj*iG LOS

                                           C/lTALfTJC OXIDATION SfSTE«

                                      WOOD RIVER NO. <» - ILLINOIS POWER CO.,

                                                  1972 TO 1973
DATE
9-1-72
9-3-72
9-6-72
9-7-72
9-11-72
9-12-72
9-15-72
9-11-72
9-15-72
9-16-72
9-17-72
9-18-72
9-19-72
9-2H-72
10-6-72
10-7-72
HOURS
12
2*
21
2
2
16
21
21
2*
21
21
21
3
17
12
21
 MOTE*  THE OPERATION T1«C LOS DOES NOT INCLUDE INT

EHWITTNET SYSTEM OPERATION DURING 1971.  SYSTEM

OPERATIONS FOR 1971 AMOUNTED TO 55 HRS.  TO

TAL OPERATION TIME FOR  2.5  TRS. OF OPERATION WAS

657 HRS.
                                                            287
                                                                                      PEDCo  ENVIRONMENTAL.
                                                                                             CINCINNATI. OHIO 45246

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                 TABLE 16
 TERMINATED FGU SYSTEMS        06/77
IDENTIFICATION NO.
UTILITY NAME
UNIT NAME
UNIT LOCATION
UNIT RATING
FUEL CHARACTERISTICS
F6D VENDOR
PROCESS
NEW OR RETROFIT
START UP DATE
F6D STATUS
EFFICIENCY,
 PARTICULATES
  10
 KEY WEST UTILITY BOARD
 STOCK ISLAND PLANT
 KEY MEST FLORIUA
   37 MW
 OIL 2.4 PERCENT SULFUR
 ZURN AIR SYSTEMS
 LIMESTONE SCRUBBING
 NEW
 10/72


 90 PERCENT
 S02
WATER MAKE UP
SLUDGE DISPOSAL
    PERCENT-ESTIMATED
 OPEN LOOP 2.7 GPM/MW
 UNSTABILIZEQ SLUjGE DISPOSED IN UNLINED POND
UNIT COST
* 21.6/KW CAPITAL COST
OPERATIONAL
 EXPERIENCE
 REFER TO BACKGROUND INFORMATION IN TABLE 16 OF THIS REPORT.  THIS
 FGD SYSTEM HAS BEEN OPERATIONAL SINCE OCTOBER 1972. THE FGD  SYSTEM HAS
 BEEN OUT OF SERVICE SINCE JANUARY 26,1975. MODIFICATIONS AND REPAIRS ARE
 CURRENTLY IN PROGRESS. SYSTEM RESTART IS STILL INDEFINITE. A CHECKOUT
 OF ALL SYSTEM MOTORS AND PUMPS MUST BE COMPLETED BEFORE STARTUP CAN
 COMMENCE. DURING THE REPORT PERIOD THE UNIT DID NOT OPERATE  BECAUSE OF
 REPAIRS TO BOILER TUBES THAT FAILED. RESTART IS SCHEDULED SHORTLY.
                                                           268
                                                                                        PEDCo  ENVIRONMENTAL
                                                                                               CINCINNATI. OHIO

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                                                      BACKGROUND INFORMATION

                                                                ON

                                                        STOCK ISLAND PLANT

     THE UTILITY BOARD OF THE CITY OF KEY WEST OWNS AND OPERATES A NEW 37-HW OIL-FIRED POWER BOILER. INSTALLED AT THEIR STOCK

ISLAND PLANT WHICH IS LOCATED DIKECTLY ADJACENT TO THE ISLAND CITY OF KLY WEST.  THE BOILEK IS AN ERIE CITY BALANCED-DRAFT OIL-

FIRED UNIT THAT IS NOMINALLY RATED AT 37 «W AND CAN ACHIEVE HZ MW AT FULL PERFORMANCE.  THE UNIT FIRLS NO. 6 RESIDUAL FUEL OIL

FROM VENEZUELA WITH SULFUR AND ASH CONTENTS OF 2.75 AND 0.05 PERCENT. RESPECTIVELY. THE UNIT'S GROSS HEAT RATE IS 11,300

BTU/KWH.  INITIAL OPERATION OF THE UNIT COMMENCED IN NOVEMBER 1972.

     THE EMISSION CONTROL SYSTEM FOR THIS UNIT CONSISTS OF A MULTIPLE TUBE MECHANICAL DUST COLLECTOR INSTALLED UPSTREAM OF TWO

SULFUR DIOXIDE WET SCRUBBERS DESIGNED AND INSTALLED BY ZURN AIR INDUSTRIES.  THIS IS A DEMONSTRATION FACILITY (EPA FUNDED)

EMPLOYING LIMESTONE IN A SEAWATER SOLUTION FOR THE REMOVAL OF SULFUR DIOXIDE FROM THE BOILER FLUE GAS STREAM.  NO PROVISIONS FOR

STACK 6AS REHEAT EXIST AT THE FACILITY.

     THE LIMESTONE ABSORBENT IS OBTAINED FROM CORAL DREDGED FROM THE OcEAN.  THE CORAL CONSISTS PRIMARILY OF CAC03 WITH LITTLE OR

NO MGC03.  THE CORAL IS GROUND TO A FINE POWDER IN A HAMMERMILL CRUSHER TO 90 PERCENT MINUS 325 MESH AND SLURRIED IN SEAWATCR.

     ZURN DUSTRAXTORS ARE EMPLOYED FOR THE REMOVAL OF SULFUR DIOXIDE AND RESIDUAL PARTICIPATE FROM THE BOILER FLUE GAS.  THE TWO

SCRUBBER MODULES ARE DESIGNED TO HANDLE A COMBINED TOTAL OF 126,9bO CFM AT ISO F.  FLUE GASES FROM THE BOILER ARE DRAWN THROUGH AN

INDUCED DRAFT FAN AND FORCED EITHER THROUGH THE BYPASS DUCT OR THROUGH ONE OR BOTH SCRUBBERS VIA THREE SETS OF DAMPERS BETWEEN THE

INDUCED-DRAFT FAN AND THE STACK.  BEFORE ENTERING THE SCRUBBING SYSTEM THE GAS IS COOLED FROM 360 F TO 160 F BY SEAWATER SPRAYS.

THIS COOLING PROTECTS THE FIBERGLASS COMPONENTS OF THE SCRUBBER MODULES.  A PRESSURE DROP OF 12 TO m INCHES WATER GAUGE IS THE

NORMAL OPERATING RANGE FOR THE SCRUBBERS.  THE SPENT SCRUBBING SLURRY IS BLED OFF TO TWO ON-SITE SETTLING PONDS WITH A RETENTION

CAPACITY OF 21 DAYS.  THE SLUUGE SETTLES OUT AND CLARIFIED WATER IS DISCHARGED BACK INTO THE SEA BY AN OVERFLOW PIPE AND SEEPAGE.

THE PARTICULATE AND SULFUR DIOXIDE REMOVAL EFFICIENCIES OF THE EMISSION CONTROL SYSTEM ARE 6* TO e2 PERCENT AND 69 TO 73 PERCENT.

RESPECTIVELY.  ACTUAL INLET AND OUTLET SULFUR DIOXIDE LOADINGS ARE 1300 TO 1500 PPM AND 300 TO 500 PPM.  INLET AND OUTLET PARTI-

CULATE LOADINGS ARE 0.20 GR/SCF AND 0.05 GR/SCF.
                                                               289                '(   '  ^ PEDCo  ENVIRONMENTAL
                                                                                                   CINCINNATI. OHIO 45246

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STOCK ISLAND (CONTINUED)

SYSTEM PERFORMANCE

     START-UP OF THE  SCRUBBING  SYSTEM  OCCURRED  IN  AUGUST  1973.   ENSUING  OPERATION  HAS  PROCEEDED ON  AN  INTERMITTENT  BASIS.   THE
                                             •
MAJOR PROBLEM AREAS ENCOUNTERED HAVE INCLUDED*

     SEVERE CORROSION OF  GAS  QUENCH DUCT  AND  DAMPER  SEALING FANS ON  INLET  AND  OUTLET OF  SCRUBBERS.

     PLUGGING AT THE  BOTTOM OF  SCRUBBER TUBES.

     LIQUID LEVEL CONTROL FAILURES  IN  THE SCRUBBER MODULES.

     POOR LIMESTONE UTILIZATION I APPROXIMATELY  20  PERCENT).

     INDUCED DRAFT FAN REPAIRS.

     REPLACEMENT OF INTERNAL  STAINLESS STEEL  PARTS WITH MONEL COMPONENTS.

     BOILER FOUNDATION AND BOILER TUBE PKOBLEMS.

     LIMESTONE SUPPLY SHORTAGES.

     ADDITIONAL INFORMATION AND DETAILS ON THE  PROGRESS OF  THIS  INSTALLATION ARE PRESENTED IN THE PERFORMANCE TABLE BELOW.

A PROCESS FLOW DIAGRAM IS PRESENTED  IN FIGURE 13 OF  APPENDIX C.
                                                               290
                                                                                            PEDCo  ENVIRONMENTAL
                                                                                                  CINCINNATI. OHIO

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                                                      STOCK  ISLAND  fCONTINUED)
                OPERATING HOURS           FGD SYSTEM
MONTH        BOILER      FGD SYSTEM      AVAILABILITY                           COMMENTS
                                                            FGD SYSTEM WAS SHUT DOWN ON JANUARY 26,  1975,  BECAUSE OF DAMAGED
                                                            DUCTWORK  BAFFLES.  SPRAY TREES AND OTHER STAINLESS STEEL PARTS HAVE
                                                            BEEN REPLACED WITH MONEL.
JUL. 75                                                     FGO SYSTEM IS STILL OUT OF SERVICE BUT IS SCHEDULED FOR RESTART IN
                                                            EARLY OCTOBER.
AU6. 75                                                     BOILEH HAS BEEN DOWN SINCE AUGUST 30 FOR REPAIRS OF THE INDUCED-DRAFT
                                                            FAN.
SEP. 75                                                     FGD SYSTEM IS STILL OUT OF SERVICE.  DATE OF SYSTEM RESTART IS
                                                            INDEFINTE.
OCT. 75
NOV. 75                                                     FGD SYSTEM IS STILL OUT OF SERVICE.  THE UTILITY IS REPLACING DAMPERS
DEC* 75                                                     AND VARIOUS SYSTEM PARTS.  DATE OF SYSTEM RESTART IS STILL INDEFINITE.
JAN. 76                                                     REPAIRS TO OUTLET DAMPER ARE COMPLETE.  ALL HOLES IN THE HOPPER HALL
FEB. 76                                                     AND DUCTWORK HAVE BEEN PATCHED.  NEW SPRAY TREES HAVE BEEN INSTALLED.
                                                            THE SYSTEM WILL NOT BE PLACED IN SERVICE UNTIL A THOROUGH CHECKOUT
                                                            OF ALL THE PUMPS AND MOTORS IS FIRST COMPLETED.
MAR. 76                                                     THE FGO SYSTEM RESTART HAS BEEN DELAYED BECAUSE OF BOlLER.REi.ATED
APR. 76                                                     PROBLEMS.  DATE OF SYSTEM RESTART IS STILL INDEFINITE.
MAY  76                                                     THE UTILITY REPORTED THAT REPAIRS AND MODIFICATIONS ARE NEARING
                                                            COMPLETION.
JUN. 76                                                     SYSTLM RESTART IS EXPECTED SHORTLY.
                                                               291
                                                                                            PEDCo  ENVIRONMENTAL
                                                                                                  CINCINNATI. OHIO 45246

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                                                    STOCK ISLAND (CONTINUED)

                OPERATING HOURS           FGD SYSTEM
MONTH        BOILER      FGD SYSTEM      AVAILABILITY                           COMMENTS

JUL. 76                                                    ALL MODIFICATIONS TO THE SCRUBBING SYSTEM WHICH CAN BE MADE AT THE

AUG. 76                                                    PRLSENT TIME HAVE BEEN COMPLETED.  THE SCRUBBING SYSTEM HAS BEEN

                                                           SEALE.D OFF FROM THE BOILER BY A METAL PARTITION WHILE THE MODIFICA-

                                                           TIONS WERE IN PROGRESS.  FINAL MODIFICATIONS CAN BE COMPLETED ONLY

                                                           WHEN THE SCRUBBING SYSTEM AND BOILER HAVE BEEN INTEGRATED INTO ONE

                                                           UNIT, WHICH WILL REQUIRE BRINGING THE BOILER DOWN.  THE UNIT IS

                                                           CONTINUING TO FIRE 2.1-2.4 PERCENT SULFUR FUEL OIL.

SEP. 76                                                    THE BOILER HAS BEEN TAKEN OUT OF SERVICE BECAUSE OF TUBE FAILURES.

OCT. 76                                                    THE METAL PARTITION BETWEEN THE SCRUBBING SYSTEM AND BOILER HAS

                                                           BEEN REMOVED.  A SHAKE-DOWN AND TEST RUN ON WATER WILL BE CONDUCTED

                                                           SHORTLY.

NOV. 76                                                    THE UTILITY REPORTED NO CHANGE IN STATUS, REPLACEMENT PARTS HAVE

DEC. 76                                                    JUST REACHED THE PLANT. TENTATIVE RESTART DATE IS FEB. If 1977.

JAN. 77     DURING THIS REPORT PERIOD. STOCK ISLAND IS BEING

FEB. 77     REMOVED FROM THE OPERATIONAL SYSTEMS TABLE.

MAR. 77     IT HAS NOT YET  BEEN DECIDED WHETHER THERE  WILL

            BE FUTURE FGD OPERATIONS AT THE UTILITY.
                                                                                           PEDCo   ENVIRONMENTAl
                                                                                                  CINCINNATI, OHIO 45246

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STOCK ISLAND PLANT

PERFORMANCE  HISTORY
PERIOD TOTAL PERIOD (MRS)
SEP.
OCT.
NOV.
DEC.
JAN.
FEB.
HAR.
APR.
HAY
JUN.
JUL.
AUG.
SEP.
OCT.
NOV.
DEC.
JAN.
FEB.
MAR.
APR.
HAY
JUN.
JUL.
AUG.
72
72
72
72
73
73
73
73
73
73
73
73
73
73
73
73
7*
7*
7%
7«»
7*
7*
7«»
7*
696
7
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                                                     STOCK ISLAND PLANT
                                               PERFORMANCE HISTORY 
AUG.
SEP.
OCT.
NOV.
DEC.
JAN.
FEB.
MAR.
APR.
MAT.
JUN.
JUL.
AUG.
7*
7*
74
7*
74
75
75
75
75
75
75
75
75
840
672
672
840
672
672
840
672
672
840
672
672
840
641
36
672
840
672
672
642
672
672
840
672
672
160
SCRUBBER (HKS)
216
0
252
362
108
110
0
0
0
0
0
0
0
OPERABII
34
0
38
43
16
16
0
0
0
0
0
0
0
TOTAL
26880
20895
                                                     1579
                                                                                       PEDCo  ENVIRONMENTAL
                                                                                              CINCINNATI. OHIO

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                 TABLE K,
 TERMINATED FGU SYSTEMS
          06/77
IDENTIFICATION NO.

UTILITY NAME

UNIT NAME

UNIT LOCATION

UNIT RATING

FUEL CHARACTERISTICS

FGO VENDOR

PROCESS

NEW OR RETROFIT

START UP DATE

F6D STATUS

EFFICIENCY,
 PARTICULATES



 S02
  11

POTOMAC  ELECTRIC & POWER

OICKERSON  NO.  3

OICKERSON  MARYLAND

   95  MM

COAL    2.0 PERCENT SULFUR

CHEHICO

MAGNESIUM OXIDE  SCRUBBING

RETROFIT

  9/73
 99.3 PERCENT
 90 PERCENT
 WATER  HAKE UP
 3.2 GPM/MW
 SLUDGE  DISPOSAL
 UNIT  COST
S70/KU CAPITAL
 OPERATIONAL
 EXPERIENCE
 REFER TO BACKGROUND INFORMATION  SECTION  IN  TABLE  i&  OF  THIS  REPORT.   THIS
 FGO SYSTEM HAS BEEN OPERATIONAL  SINCE  SEPTEMBER 1973. THE  UNIT HAS BEEN
 TERMINATED AS AN S02 SCRUBBER. HOWEVER,  IT  WILL CONTINUE TO  OPERATE  AS  A
 PARTICULATE SCRUBBER.
                                                           295
                                                                                        PEDCo  ENVIRONMENTAL
                                                                                              CINCINNATI. OHIO

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                                                       BACKGROUND INFORMATION
                                                                ON
                                                           DICKERSON NO.  3
     THE DICKERSON STATION OF POTOMAC ELECTRIC POWER CO. (PEPCO) IS LOCATED ON THE POTOMAC RIVER NEAR DICKERSONt MARYLAND. ABOUT
SO MILES NORTHWEST OF WASHINGTON, O.C.  THE STATION HAS 3 ELECTRIC GENERATORS, EACH RATED AT 190 MW.  UNIT NO. 3 IS A DRY BOTTOM
COAL-FIRED BOILER DESIGNED BY COMBUSTION ENGINEERING AND INSTALLED IN 1962.  THE COAL NOW BURNED HAS AN AVERAGE GROSS HEATING
VALUE OF 11,700 BTU/LB AND AVERAGE ASH AND SULFUR CONTENTS OF l
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                                                           OICKCRSOH IVO. 3
                                                    FGD  SYSTCH  OPERATING  HlSTOHV

OPERATING PERIOD                                                 COMMENTS

SEP. 73            PROBLEMS DURING THIS PERIOD RANGED FROM CORROSION LEAKS IN EXPANSION JOINTS TO PROBLEMS IN MATERIAL

  10               HANDLING EQUIPMENT FEEDING AND SLAKING OF MGOt PLUGGING IN THE MGO MIX TANK AND SUCTION LINES TO THE

JAN. 71            MGO MAKE-UP PUMPS.

J*N» ™            MAINTENANCE AND MODIFICATIONS MERE PERFORMED ON THE SYTSTEM.  THE MAJOR SYSTEM REVISION HADE DURING

  TO               THIS PERIOD MAS THE ADDITION OF A PRE-MIX TANK IN THE MGO SYSTEM.


APR. 70

APR. 7*            LIMITED OPERATION BECAUSE THE UTILITY DID NOT HAVE ACCESS TO THE EPA CALCINING FACILITY AT THE ESSEX

  TO               CHEMICAL COMPANY SULFURIC ACID PLANT.  BY THE END OF JUNE 197<». ALL THE MGO AT DlCKERSON HAD BEEN USED

JUL. 74            AND A SILO PLUS THREE CARS HERE FULL OF MGS03.

AU6. 71            DURING THIS PERIOD THE SYSTEM GENERALLY OPERATED AT 75 PERCENT OF THE DESIGN GAS FLOM.

  TO

DEC. 7*

JAN. 75            PROBLEMS DEVELOPED IN THE BUCKET ELEVATOR TRANSPORTING THE M6S03 FROM THE DRYER TO THE STORAGE SILO.

FEG. 75            UNIT NO. 3 HAS TAKEN OUT OF SERVICE FOR AN 6 TO 12 WEEK TURBINE OVERHAUL.  THE SCRUBBER UAS INSPECTEDt

  TO               MAINTENANCE AND MODIFICATIONS MERE MADEt

JUL. 75

AUG. 75            THE F6D SYSTEM WAS RESTARTED IN AUGUST. STEAM MAS LOST TO THE MGO MIX TANK, RESULTING IN A VERY MOIST

                   PRODUCT FROM THE CENTRIFUGE.  CAKING IN THE DRYER OCCURED.  AT THIS POINT, THE UTILITY DECIDED TO TEST

                   ONLY THE FIRST-STAGE OF THE SCRUBBING SYSTEM, TAKING GAS AHEAD OF THE PgECIPITATOR.  FGD OPERATION AT

                   DlCKERSON TERMINATED AT THIS POINT.
                                                               297
                                                                                           PEDCo  ENVIRONMENTAL
                                                                                                  CINCINNATI. OHIO 45246

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                 TABLE; i
 TERMINATED F6U SYSTEMS
         06/77
IDENTIFICATION NO.
UTILITY NAME
UNIT NAME
UNIT LOCATION
UNIT RATING
FUEL CHARACTERISTICS
F60 VENDOR
PROCESS
NEW OK RETROFIT
START UP DATE
F6D STATUS
EFFICIENCY,
 PARTICULATES
 12
PUBLIC SERVICE CO OF COLORADO
VALMONT NO. 5
VALMONT COLORADO
  so nw
COAL 0.72 PERCENT SULFUR
UOP/PUB SERVICE OF COLORADO
LIMESTONE SCRUBBING
RETROFIT
10/7*
95 PERCENT
 S02
05 PERCENT
WATER HAKE UP
CLOSED LOOP
SLUDGE DISPOSAL
UNSTABILIZED SLUoGE DISPOSED IN LINED POND
UNIT COST
OPERATIONAL
 EXPERIENCE
REFER TO BACKGROUND INFORMATION IN TABLE 16 OF THIS REPORT. THIS FGD
SYSTEM HAS BEEN OPERATIONAL SINCE NOVEMBER 1V7"». THE FGD SYSTEM
TERMINATED AT THIS STATION IS AN EXPERIMENTAL UNIT, ORIGINALLY DESIGNED
BY UNIVERSAL OIL PRODUCTS FOR PARTICIPATE REMOVAL ONLY. ONE OF THE TWO
PARALLEL SCRUBBING MODULES MAS CONVERTED TO LIMESTONE SCRUBBING FOR
EXPERIMENTAL PURPOSES ONLY.
                                                           298
                                                                                        PEDCo  ENVIRONMENTAL
                                                                                              CINCINNATI. OHIO

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                                                     BACKGROUND INFORMATION
                                                                ON
                                                          VALMONT NO.  5
     THE VALMONT POWER STATION OF THE PUBLIC SERVICE COMPANY OF COLORADO is LOCATED IN VALMONT,  COLORADO,  APPROXIMATELY  20  MILES
NORTH OF DENVER.  VALMONT NO. 5 IS A COAL-FIRED UNIT THAT FIRES GAS A  FEW MONTHS DURING THE YEAR.   THE  COAL GENERALLY
EMPLOYED FOR THIS UNIT IS WYOMING ROSEBUD, WHICH HAS AN AVERAGE GROSS  HEATING VALUE OF 10.760 BTU/LB WITH  ASH CONTENT  IN THE 6 TO
7 PERCENT RANGE AND SULFUR CONTENT LESS THAN 1 PERCENT.
     THE F6D SYSTEM BEING TESTED AT THIS STATION IS AN EXPERIMENTAL UNIT ORIGINALLY DESIGNED BY UNIVERSAL  OIL PRODUCTS FOR  PANIC-
ULATE REMOVAL ONLY.  THIS TCA UNIT CONSISTS OF TWO PARALLEL MODULES WITH A COMBINED CAPABILITY OF  TREATING APPROXIMATELY 90
PERCENT OF THE TOTAL FLUE GAS LOAD OR THE EQUIVALENT OF APPROXIMATELY 100 «W GENERATING CAPACITY (50 HW PER MODULE}.   THIS  SYSTEM
WAS COMPLETED AND OPERATIONAL IN 1971 AND RAN UNTIL OCTOBER 197*».  PARTICULATE REMOVAL EFFICIENCY  WAS MEASURED AT 95  PERCENT,
SULFUR DIOXIDE REMOVAL EFFICIENCY WAS «5 PERCENT, AND AVAILABILITY WAS APPROXIMATELY 70 PERCENT.  FREQUENT SCRUBBER OUTAGES WERE
CAUSED PRIMARILY BY SUPERSATURATED CALCIUM SULFATE IN THE SCRUBBING LIQUOR.  TO MINIMIZE CLEANOUTS AND RECTIFY SCALING PROBLEMS.
A PH CONTKOL PROGRAM WAS IMPLEMENTED FOR ONE OF THE SCRUBBING MODULES WITH ADDITION OF LIMESTONE TO THE SCRUBBING LIQUOR.  THIS
MODIFICATION WAS EXPECTED TO MINIMIZE SCALING, DECREASE SCRUBBER OUTAGES FOR CLEANOUTS. AND INCREASE AVAILABILITY. THE EXPECTED
RESULTS DID NOT MATERIALIZE.  SCALE BUILDUP CONTINUED AND AVAILABILITY DECREASED.  TESTS DURING THE PH CONTROL PROGRAM SHOWED
PARTICULATE REMOVAL EFFICIENCY AT 95 PERCENT.  SULFUR DIOXIDE REMOVAL EFFICIENCY INCREASED TO 85 PERCENT,  AND AVAILABILITY  DROPPED
TO 70 PERCENT.  THE UNSTABILIZED SLUDGE GENERATED DURING THIS OPERATION MAS PUMPED TO A LINED POND.  THE OPERATIONAL  DATA GENER-
ATED FROM THE LIMESTONE MODIFICATION PROGRAM ARE PRELIMINARY. BASED UPON A 4.5 MONTH TESTING PROGRAM.
                                                               299
                                                                                  "     ^ PEDCo  ENVIRONMENTAL
                                                                                                   CINCINNATI. OHIO 45246

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                                                                VALMONT  NO.  5
               OPERATING HOURS           F6D SYSTEM
RONTH      BOILER     FGD SYSTEM       OPERABlLlTY (X)                                COMMENTS
SEP. 75                                                     THIS FACILITY HAS BEEN INACTIVE SINCE SEPTEMBER  1.  1975.  BECAUSE OF A
OCT. 75                                                     TURBINE  GENERATOR FAILURE.   THt UNIT IS SCHEDULED TO GO ON LINE AGAIN
NOV. 75                                                     IN DECEMBER  1975.  THIS UNIT IS STILL INACTIVE BECAUSE OF A BOILER
DEC. 75                                                     OVERHAUL.  THE SCNUBBER/ABSORBEK TRAIN IS AVAILABLE AND WILL BE COUPLED
                                                            INTO THE SYSTEM  WHEN THE BOILER GOES BACK ON-LINE.
JAN. 76                                                     THE BOILER OVERHAUL HAS BEEN COMPLETED.  THE UNIT IS AVAILABLE IN THE
FEB. 76                                                     PARTICULATE  REMOVAL MODE ONLY.  THE UTILITY IS SUSPENDING RESUMPTION
                                                            OF THE LIMESTONE MODIFICATION OPERATION FOR AN INDEFINITE PERIOD.
MAR. 76                                                     THE EXPERIMENTAL LIMESTONE  SCRUBBING PROGRAM HAS INACTIVE DURING THE
APR. 76                                                     REPORT PERIOD.  RESUMPTION  OF THE PROGRAM IS CONSIDERED INDEFINITE AT
MAY  76                                                     THE PRESENT  TIME.THE EXPERIMENTAL LIMESTONE SCRUBBING PROGRAM REMAINED
JUN* 76                                                     INACTIVE DURING  THE REPORT  PEKIOD.  PRESENT PLANS CALL FOR THE RESUMP-
JUL. 76                                                     TION OF  THIS PROGRAM SOMETIME IN THE FALL OF 1976.  THE TCA UNIT IS
AUG. 76                                                     NOW OPERATIONAL  IN THE PARTICULATE REMOVAL MODE.  THE NO. 5 UNIT FIRES
                                                            A COMBINATION OF COAL AND NATURAL GAS MEETING CURRENT STATE AIR
                                                            EMISSION STANDARDS.
SEP. 76                                                     NO CHANGE  IN STATUS.  THE RESUMPTION OF THE EXPERIMENTAL LIMESTONE
OCT. 76                                                     ADDITIONAL AND S02 REMOVAL  PROGRAM IS STILL INDEFINITE.  THE TCA
                                                            MODULES  ARE  CONTINUING TO OPERATE IN THE PARTICULATE REMOVAL MODE.
                                                            CARRYOVER  INTO THE RECIRCULATION SYSTEM IS STILL A PROBLEM AREA.
                                                            THE LOW  PH SCRUBBER ENVIRONMENT HAS CAUSED A MATERIALS PROBLEM,
                                                            NECESSITATING REPLACEMENT OF 30H SS PARTS WITH 316 SS.
NOV. 76                                                     THE UTILITY  HAD  NO CHANGE IN STATUS TO ANNOUNCE FOR THE
DEC. 76                                                     CURRENT  REPORT PERIOD.
                                                               300
                                                                                           PEDCo  ENVIRONMENTAL
                                                                                                  CINCINNATI. OHIO

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                                                   VALMONT NO.5 (CONTINUED)

               OPERATING HOURS           FGD SYSTEM
MONTH      BOILER     FGD SYSTEM       OPEHABILITY (X)                                COMMENTS
                                                            PARTICULATL-REMOVAL  OPERATIONS  ARE  STILL  IN PROGRESS. THE CONTINUATION

                                                            OF  ANY  FUTURE FGD  OPERATIONS  IS CONTINGENT UPON  REGULATORY DECISIONS.
                                                               301
                                                                                            PEDCo  ENVIRONMENTAL
                                                                                                   CINCINNATI. OHIO

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                 TABLE; i&
  TERMINATED FGU SYSTEMS        06/7T
 IDENTIFICATION NO.

 UTILITY NAME

 UNIT NAME

 UNIT LOCATION

 UNIT RATING
  13

 SOUTHERN CALIFORNIA EDISON

 MOHAVE NO 1A

 LAuGHLIN NEVADA

  170 HW
FUEL CHARACTERISTICS  COAL  0.5 - 0.6 PERCENT SULFUR
FGO VENDOR

PROCESS

NEW OR RETROFIT

START UP DATE

FGD STATUS

EFFICIENCY.
 PARTICIPATES
 UNIVERSAL OIL PRODUCTS

 LIMESTONE SCRUBBING

 RETROFIT

 11/7H





 93 PERCENT
 S02
WATER HAKE UP
 95 PERCENT


 0.92 GPM/MW
SLUUGE DISPOSAL
UNIT COST
NOT AVAILABLE
OPERATIONAL
 EXPERIENCE
 THIS EXPERIMENTAL MODULE STARTED UP OCT. 31. 197* AND OPERATED WITH AN
 AVAILABILITY OF fc0.i»* THROUGH FOUR MONTHS OF TESTING.  TEST HAVE BEEN
 COMPLETEo« AND THE F&O SYSTEM WAS SHUT DOWN INDEFINITELY ON JULY 2, 1975.
 NEVADA ASSEMBLY BILL NO. ?oe HAS PLACED A TWO YEAH MORATORIUM ON THE
 ENFORCEMENT OF THE COMPLIANCE SCHtDULE FOR THIS STATION.  FURTHER FGO
 ACTIVITIES WILL BE DEPENDENT ON FUTURE LEGISLATION.
                                                           302
                                                                                        PEDCo  ENVIRONMENTAL
                                                                                               CINCINNATI. OHIO

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                 TABLE 16
 TERMINATED FGU SYSTEMS
         Ob/77
IDENTIFICATION NO.
UTILITY NAME
UNIT NAME
UNIT LOCATION
UNIT RATING
FUEL CHARACTERISTICS
FGD VENDOR
PROCESS
NEW OR RETROFIT
START UP DATE
FGO STATUS
EFFICIENCY.
 PARTICIPATES
 It
SOUTHERN CALIFORNIA EDISON
HOHAVE NO. 2A
LAUGHLIN NEVADA
 160 MM
COAL  0.5-0.6 PERCENT SULFUR
SCE/STEARNS KOGER
LIME SCRUBBING
RETROFIT
11/73
 93 PERCENT
  S02
 WATER PAKE UP
 SLUDGE DISPOSAL
                       95  PERCENT
 1.0 6PH/HU
  STABILIZED SLUDGE DISPOSED IN  UNLINED  POND
 UNIT COST
 OPERATIONAL
  EXPERIENCE
NOT AVAILABLE
 SINCE STARTUP OF FORMAL TEST  PROGRAM  ON  JANUARY  16.  197H«  AND  UP  TO  DEC-
 EMBER 20.197U. THIS EXPERIMENTAL  HORIZONTAL  MODULE OPERATED  5260  HRS.
 WITH AN OVERALL AVAILABILITY  OF 77.«»  PERCENT,  S02 REMOVAL  WAS  90  PERCENT
 IN FLUE GAS TO SIMULATE CONDITIONS FROM  COMBUSTION OF  HIGH-SuLFUK COAL.
 THIS FGD SYSTEM OPERATED FROM NOVEMBER 1973  UNTIL FEBRUARY 1975.   THE
 UTILITY HAS NO CURRENT PLANS  FOR  FGD  AT  ANY  OF ITS PLANTS.
                                                           303
                                                                                        PEDCo  ENVIRONMENTAL
                                                                                               CINCINNATI. OHIO 45246

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                                                   BACKGROUND INFORMATION

                                                            ON

                                        THE MOHAVE TEST MODULES PROGRAM:  NOS. 1A AND 2A


     TWO PROTOTYPE SULFUR DIOXIDE ABSORBER MODULES WERE INSTALLED IN  1973 AT THE MQHAVE GENERATING STATION OF THE  SOUTHERN  CAL-

IFORNIA EDISON COMPANY.  A VERTICAL MODULE, RATED AT 170 MW, WAS INSTALLED  TO TREAT 450.000 SCFM PORTION OF  THE FLUE  GAS  FROM

UNIT NO. 1. A HORIZONTAL MODULE. ALSO RATED AT 170 MW, WAS  INSTALLED  TO TREAT A  SIMILAR FLUE GAS PORTION FROM UNIT NO.  2.   UNITS

1 AND 2 ARE IDENTICAL BOILERS, EACH HAVING A MAXIMUM NET CONTINUOUS GENERATING CAPACITY OF 790 NW AND EACH BURNING A  WESTERN,  LOW.

SULFUR COAL WITH A HEATING VALUE OF 11.900 BTU/LB AND ASH AND SULFUR  CONTENTS OF 10 AND 0.4 PERCENT RESPECTIVELY.

VERTICAL MODULE

     THE VERTICAL MODULE, A UNIVERSAL OIL PRODUCTS TURBULENT CONTACT  ABSORBER 
-------
                           MOHAVE NO. 1A - VEKTICAL TEST MODULE



                  OUTAGE TIME HISTORY*  NOVEMBER 2. 197«t TO JULY 2. 1975




                    REASON                                   TIME (HR1



1.   REPAIR 6RIDS AND REDISTRIBUTE TCA BALLS                    710



2.   CLEAN SCALE FROM SCRUBBER INTERNALS                        3«»«»




3.   REPAIR/REPLACE PLUGGED NOZZLES                             153



«.   REPAIR LEAKS IN TRAP-OUT TRAY                              120




5.   REPAIR/REALIGN PPA PACKING                                  65



6.   CORRECT BOOSTER FAN TRIP PROBLEMS                           72



7.   CONDUCT INSPECTIONS FOR EXTENDED OPERATIONS                 
-------
                           MOHAVE  NO.  2A  -  HORIZONTAL  TEST MODULE
                 OUTAGt  TIME  HISTORY*   JANUARY  l6t  197*  TO FEBRUARY 9. 1975
                     KEASON                                      TINE (HR)
 i.   MODIFY AND REPAIR  PLASTIC  OEMISTER  BLADES                     503
 2.   CORRECT BOOSTER FAN BALANCE  PROBLEMS                          317
 3.   PUMP REPAIR                                                   256
 4.   SPRAY NOZZLE REPLACEMENT                                       236
 5.   MODIFY 6AS INLET FLOW DISTRIBUTION                             162
 6.   REPAIR HOPPER LEAKS                                           135
 7.   REMOVE HARDHAT FROM THICKENER                                  82
 8.   MODIFY SLAKING MATER FOR  SCALE PREVENTION                      45
 9.   CONDUCT INSPECTIONS FOR EXTENDED OPERATIONS                     19
10.   TOTAL OUTAGE TIME                                             1757
      TOTAL OUTAGE TIME*  1757  HOURS
      TOTAL CALENDER TIME* 9328 HOURS
      TOTAL OPERATING TIME*  7571  HOURS
      PERCENT AVAILABILITY*  81.16*
                                            306
                                                                        PEDCo  ENVIRONMENTAL
                                                                               CINCINNATI. OHIO 45246

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                 TABLE 16
 TERMINATED FGU SYSTEMS
         06/77
IDENTIFICATION NO.

UTILITY NAME

UNIT NAME

UNIT LOCATION

UNIT RATING

FUEL CHARACTERISTICS

FGO VENDOR

PROCESS

NEW OK RETROFIT

START UP DATE

FGO STATUS

EFFICIENCY.
 P ARTICULATES
 15


TENNESSEE VALLtY AUTHORITY


SHAWNEE NO.  IOC


PADUCAH KENTUCKY


  10 MW


COAL 2.9 PERCENT SULFUR


TENNESSEE VALLEY AUTHORITY


LIRE/LinESTONE SCRUBBING


RETROFIT
EXPERIMENTALLY CONTROLLED
 S02
EXPERIMENTALLY CONTROLLED
WATER HAKE UP
EXPERIMENTALLY CONTROLLED
SLUDGE DISPOSAL
UNIT COST
OPERATIONAL
 EXPERIENCE
REFER TO BACKGROUND INFORMATION SECTION IN TABLE 16.  THIS
FGD SYSTEM HAS BEEN OPERATIONAL SINCE APRIL.1972.  THIS MARBLE-BED AB-
SORBER. MANUFACTURED BY COMBUSTION ENGINEERING CO.. WAS DISCONTINUED
EARLY IN THE TEST PROGRAM BECAUSE OF CONTINUED OPERATING PROBLEMS WITH
NOZZLE FAILURE AND SUBSEQUENT PLUGGING OF THE MARBLE BED.  THIS SYSTEM
BECAME OPERATIONAL IN APRIL 1972 AND HAS PERMANENTLY TERMINATED IN
JULY 1973.
                                                           307
                                                                                         PEDCo  ENVIRONMENTAL

                                                                                                CINCINNATI. OHIO 45246

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                                                  BACKGROUND INFORMATION
                                                          ON
                                              SHAWNEE NOS. 10A, 108, AND IOC
     IN JUNE 1968i  THE EPA INITIATED A PROGRAM TO TEST PROTOTYPE WET LIME AND LIMESTONE SCRUBBING SYSTEMS FOR REMOVAL OF SULFUR
DIOXIDE AND PARTICULATES FROM FLUE GAS.  THE PROGRAM WAS CARRIED OUT IN A TEST FACILITY INCORPORATED INTO THE FLUE GAS DUCT WORK
OF UNIT NO. 10, A COAL-FIRED BOILER AT THE TVA SHAWNEE POWER STATION. PAOUCAH, KENTUCKY.  TVA IS THE CONSTRUCTOR AND FACILITY
OPERATOR AND THE BETCHEL CORP. IS THE MAJOR CONTRACTOR AND TEST DIRECTOR.
     THE TEST FACILITY CONSISTS OF THREE PARALLEL SCRUBBER SYSTEMS OF PROTOTYPE SIZE TREATING PART OF TH£ FLUE GAS FROM THE
BOILER.  EACH SCRUBBER TRAIN IS CAPABLE OF TREATING APPROXIMATELY 30.000 ACFM, OR THE EQUIVALENT OF APPROXIMATELY 10 MW OF POWER
PLANT GENERATING CAPACITY.
     THREE PARALLEL WET SCRUBBER SYSTEMS WERE SELECTED FOR THE TEST PROJECT* u A VENTURI WITH A SPRAY TOWER AFTER ABSORBER* 21 A
TURBULENT CONTACT ABSORBER (TCA) AND 3) A MARBLE-BED ABSORBER.  THE VENTURI SYSTEM, MANUFACTURED BY CHEMICAL CONSTRUCTION CO.,
CONTAINS A" ADJUSTABLE THROAT THAT PERMITS CONTROL AND VARIATION OF PRESSURE DROP UNDER A WIDE RANGE OF FLOW CONDITIONS.  THE  TCA
UNIT, MANUFACTURED BY UNIVERSAL OIL PRODUCTS, EMPLOYS A FLUIDIZED BED OF LOW DENSITY PLASTIC SPHERES THAT ARE FREE TO MOVE BETWEEN
RETURNING GRIDS.  THE MARBLE-BED ABSORBER, SUPPLIED BY COMBUSTION ENGINEERING CO., USES A PACKING OF 3/4.INCH GLASS MARBLE
SPHERES AND A TURBULENT LAYER OF LIQUID AND GAS ABOVE THE MARBLE LAYER TO ENHANCE MASS TRANSFER.
     THE TEST FACILITY WAS DESIGNED SO THAT MODIFICATIONS A"D VARIATIONS OF SCRUBBER INTERVALS AND PIPING COULD BE READILY EMPLOY-
ED FOR EACH SCRUBBER SYSTEM.  EACH SYSTEM CAN TREAT APPROXIMATELY 30,000 ACFM OF FLUE GAS AT 300 F CONTAINING 1600 TO *000 PPM OF
SOg AND 2 TO 5 GRAINS/SCF OF PARTICULATES.  TESTING OF THE TCA AND THE VENTURI SPRAY TOWER  IS IN PROGRESS* OPERATION OF THE
MARBLE-BED ABSORBER UNIT HAS BEEN PERMANENTLY DISCONTINUED.
                                                               308
                                                                                            PEDCo  ENVIRONMENTAL
                                                                                                   CINCINNATI. OHIO 45246

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                 TABLE 16
 TERMINATED FGU SYSTEMS
         Ob/77
IDENTIFICATION NO.

UTILITY NAME

UNIT NAME

UNIT LOCATION

UNIT HATING

FUEL CHARACTERISTICS

FGD VENDOR

PROCESS

NEW OH RETROFIT

START UP DATE

FGO STATUS

EFFICIENCY,
 PARTICULATES

 S02

WATER HAKE UP

SLUDGE DISPOSAL

UNIT COST
OPERATIONAL
 EXPERIENCE
 16

UNION ELECTRIC CU.

MEREMAC NO. 2

ST. LOUIS COUNTY MISSOURI

 1HO MW

COAL   3.«» PERCENT SULFUR

COMBUSTION ENGINEERING

LlMESTONt  INJECTION/WET SCRUB

RETROFIT

 3/68




99 PERCENT


63 PERCENT


CLOSED LOOP


UNSTABILIZEO SLUuGE DISPOSED IN UNLINED POND
THE FIRST COMMERCIAL SCRUBBER APPLICATION ON A UTILITY COAL-FIRED BOILER
OCCURRED AT THIS STATION IN EARLY 19(iS. THE SCRUBBING STRATEGY INCLUDED
LIMESTONE INJECTION INTO THE FURNACE WITH AN EXISTING C"AL PULVERIZER AND
TAIL-END SCRUBBING WITH THE CALCINED REAGENT IN TWO MARBLE-BED ABSORBERS.
THIS FULL-bCALE EXPERIMENTAL SCRUBdING PROGRAM WAS EVENTUALLY TERMINATED
AND THE INSTALLATION WAS ABANDONED. PROBLEMS ENCOUNTERED INCLUDED BOILER
TUBE FOULING BECAUSE OF CLOSE TUBE SPACING. WIDESPREAD SCALING. SEVEHL
CORROSION, INEFFICIENT MIST ELIMINATOR AND PROBLEMS WITH WASTE DISPOSAL
                                                           309
                                                                                        PEDCo  ENVIRONMENTAL.
                                                                                               CINCINNATI. OHIO 45246

-------
310
                      PEDCo  ENVIRONMENTAL
                           CINCINNATI. OHIO 45246

-------
              TABLE 17

TOTAL OF FGD MEGAWATT CAPACITY BY YEAR
                   311
                                       PEDCo  ENVIRONMENTAL
                                            CINCINNATI. OHIO 45246

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312
PEDCo ENVIRONMENTAL
                            CINCINNATI. OHIO

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                 TABLE 17
TOTAL OF F6D MEGAWATT CAPACITY BY YEAR
         YEAK



         1960

         1972

         1973

         1971

         1975

         1976

         1977

         1978

         1979

         1900

         1901

         1902

         1903

         190*

         1905

         1906

         1907

      UNDEFINED
MtGAUATTS



    125

    «»27

   1*10

    250

   1051

   2200

   6751

   7330

   7361

   7103

   4965

   2303

   3735

   1250

    500

    500

    350

   2075
                                   313
                                                                 PEDCo  ENVIRONMENTAL.
                                                                       CINCINNATI. OHIO 45246

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     APPENDIX A

FGD SYSTEMS ECONOMICS
                               PEDCo ENVIRONMENTAL.
                                     CINCINNATI. OHIO 452<4e

-------
A-2
PEDCo  ENVIRONMENTAL
     CINCINNATI. OHIO 45246

-------
           APPENDIX A.   FGD SYSTEM ECONOMICS:  OPERATIONAL SYSTEMS
COMPMT
PLANT
UNITS
TOTAL CAPACITY, l*»
Arizona Public Service
Cholla Electric Generating
Station
No. 1
115


Columbus I So. Ohio Electric
Conesvllle Generating Station
No. 5
400



Cuumjnmialth Edison
Hill County Station
No. 1
167


PROCESS
STATUS
START-UP DATE
Lines tone
Operational
10/73


Line
Operational
1/77



Lines tone
Operational
2/72


REPORTED CAPITAL
COSTS,
J MILLION
6.5S5


15.27



15.542


*/KM
57.0


37.90



113


REPORTED OPERATING
COSTS.
J ANNUAL



7.765



3.985 MM


MILLS/KWH
2.20


5.61



13.06


COMMENTS
1. Capital cost figure Includes the venturl scrubbers (2)
for participate control. This figure represents
total expenditures made by the utility through 1973.
2. Capital cost figure does not Include limestone prep-
aration, sludge handling facilities and interest on
capital during construction.
3. Additional costs incurred by the system supplier have
not been reported.
4. The operating cost figure Includes operating and main-
tenance expenditures only.
1. The capital cost figure Includes direct costs only.
2. The capital cost figure Includes two scrubber nodules,
all ancillary equipment, sludge disposal system, site
preparation, and construction costs. Indirect* are
not Included.
3. Annual operating costs are estimated at a load factor
of 39.5t.
4. Annual costs Include capitalization, raw materials,
waste disposal, maintenance, labor, and utilities.
5. All cost estimates are given In 1976 dollars.
1. The capital cost figure includes the venturi scrubbers
for particulate control.
2. The t/kU figure Is based upon the unit's maximum net
generating capacity with the FGD system, 137 MU.
3. The annual operating cost figure Is based on a
system lifetime of 14 years. Sludge treatment costs
include handling to an off-site disposal area. Jhe
figure provided Is the cost to own and operate the
scrubbing system for 1975.
4. Unit load capacity factor for 1975 Mas 49.41.
Note: N/A Indicates figures are not available.
                                          A-3
                                                                    PEDCo ENVIRONMENTAL
                                                                           CINCINNATI. OHIO 45246

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APPENDIX A  (Continued).   FGD SYSTEM ECONOMICS:  OPERATIONAL SYSTEMS
COMPANY
Piwrr
IMtTC
UnlTS
TOTAL CAPACITY. MU
Duquesne Light
F.R. Phillips Station
NOS. 1 to 6
410

Elrama Station
Nos. 1 to 4
510












Kansas City Power 1 Light
La Cygne Power Station
No. 1
820






Kansas Power & Light
Lawrence Energy Center
Nos. 4 ! 5
525












PROCESS
STATUS
START-UP DATE
Line
Operational
7/73


line
Operational
10/75












Limestone
Operational
2/73







Limestone
Injection &
Met Scrubbing
Terminated,
Operational
12/68 & 11/71










REPORTED CAPITAL
COSTS.
1 MILLION
40




42














53.2









3.5















S/KH
103




93














63.9









7















REPORTED OPERATING
COSTS.
J ANNUAL



32 MM
















1.79 m









N/A















MILLS/KWH



6.0
















0.94









N/A

















COMMENTS
1. Total capital cost figure for Phillips Includes
expenditures of $32 million through 197S and an addi-
tional $8 million required to bring the entire plant
into compliance. The figure for Elrama includes
expenditures of $34 million through 1975 and an addi-
tional $12 million required to bring the entire plant
into compliance.

2. Total capital cost figures Include all process equip-
ment, engineering costs, contractor's fees and
Interest on capital during construction. Excluded
are the costs of additional sludge disposal facilities
that nay be required. The $/KW values are based upon
the station's net generating capacities with the
scrubbers in service. The Phillips station net
generating capacity is 494 MM.
3. Annual operating cost figures of 6 mllls/kWh Is based
upon the combined operating costs for the Phillips and
Elrama stations when full SO? compliance 1s achieved.
This amounts to approximately $32 million annually.
1. The capital cost figure Includes $45.4 million in
expenditures already made plus an additional $7
million required to reach optimum system performance
($5.2 million for the installation of an eighth
scrubber module).
2. The annual operating cost figures are estimates for
1976 operations based upon extrapolation of first
quarter figures provided by the utility. Included are
operating labor and materials, maintenance labor and
materials, and limestone.
1. The capital cost figure presented represents a sum
paid by the utility for both systems in 1968. Ex-
penses Incurred in many subsequent modifications
over the years were largely underwritten by the
system supplier. Therefore, the figures listed are
unreal istically low and are not meaningful.
2. These units have been and are now being replaced with
venturi rod scrubber and spray tower systems utilizing
a limestone-based scrubbing slurry.
Lawrence No. 4 rod scrubber and spray tower limestone
scrubbing system was placed in service Jan. 1977. The
original Injection unit has been dismantled.
4. Lawrence No. 5 rod scrubber and spray tower scrubbing
-*ys4«m Is now being erected. The original Injection
/VGruT^svstiH In service. Start up of the new system
/£Smi PEOC^o. JEJSIViRQrslMENTAL
Note: N/A indicates figures are not available.
                                                                      CINCINNATI. OHIO
                                       i-4

-------
   APPENDIX  A (Continued).   FGD SYSTEM ECONOMICS:   OPERATIONAL SYSTEMS
COMPANY
PLANT
UNITS
TOTAL CAPACITY, MW
Kentucky Utilities
Green River Power Station
No*. 1, 2 » 3
64

Louisville Gas S Electric
One Run Power Station
No. 4
178
Louisville Gas S Electric
Paddy Run Power Station
No. 6
65



Montana Power Co.
Colstrip Plant
Nos. 1 » 2



PROCESS
STATUS
START-UP DATE
Lime
Operational
9/75

Lime
Operational
8/76
Lime
Operational
4/73



Fly Ash/Lime
Operational
10/75 a 7/76



REPORTED CAPITAL
COSTS,
$ MILLION
3.996

10
3.7



3?. 663



t/KH
63.44

50
57



45. 3Z



REPORTED OPERATING
COSTS,
$ ANNUAL


N/A
905,000



1.185 MM



MILLS/KWH
2.0

N/A
2.5



0.26



COMMENTS
1. The capital cost figure for this turnkey Installa-
tion does not include the utility's expenditures
for engineering, operator training, and other in-
direct cost factors.
2. The operating cost figure includes operating and
maintenance expenditures only.
1. The total Installed capital cost Is an estimated
figure that includes the costs for lime handling and
sludge disposal facilities.
1. The capital cost figures are based on the boiler
rating minus system power consumption. The costs
include everything except the final waste disposal
site. This is a borrow pit supplied by the State
highway department at no cost to the utility.
2. The operating costs provided has been derived by
assuming a 601 unit load factor and a 151 fixed
charge factor.
3. Cost of the carbide lime absorbent Is confidential.
4. Costs are atypical because the unit Is used for
peak loads and the scrubber Is a research and
development tool for future full scale installations
now operational, under construction or planned by the
utility.
1. The total installed capital cost figure is an es-
timated value that includes the venturi scrubbers
installed for particulate emissions control.
2. The annual operating cost figure is an estimated
value that excludes fixed charges and solid waste
disposal operations.
3. Capital charges were not available to be Included
in the figures provided.
4. The cost figures are presented in 1975 and 1976
dollars.
Note: N/A Indicates figures are not available.
                                         A-5
                                                                   PEDCo  ENVIRONMENTAL
                                                                         CINCINNATI. OHIO 45246

-------
   APPENDIX A (Continued).   FGD  SYSTEM  ECONOMICS:  OPERATIONAL SYSTEMS
COMPANY
PLANT
UNITS
TOTAL CAPACITY, MH
Nevada Power Co.
Reid Gardner Station
Nos. ] 4 2
250

Northern Indiana Public Serv.
O.H. Mitchell Station
No. 11
115


Northern States Power
Sherbume County Generating
Plant
Nos. 1 » 2
1420



Pennsylvania Power
Bruce Hansfleld Plant
Nos. 1 * 2
1670




PROCESS
STATUS
- START-UP DATE
Sodium Carbonate
Operational
4/74

Hel Iran-Lord
Operational
6/77


Limestone
Operational
5/76 ft 5/77



Lime
Operational,
Construction
4/76 8 10/77




REPORTED CAPITAL
COSTS.
S MILLION
11

14.825


60



213.200




S/KU
44

129


44



127.66




REPORTED OPERATING
COSTS.
$ ANNUAL
1.2 MM

6.006 MM


3.77 MM



10.644 MM




MILLS/KHH
N/A

8.1






2.7




COMMENTS
1. The total installed capital cost figure is an estimate
that was originally provided by the utility for
expenditures completed by installation date (1974).
Included are both scrubbing systems along with all
the raw material handling and pond equipment cost.
2. The annual operating cost figure Includes $600,000
annualized for each unit.
1. The capital figure includes Interest during con-
struction and overhead charges.
2. Reported operating cost figure 1s a total annual i zed
cost value that includes:
0 Operation and maintenance costs.
• Anti-oxidant agent costs.
Fixed charges are calculated for a 10-15 year plant
lifetime (26X of $14,825 MH). Assume an annual unit
load factor of 73.5'-.
1. The total Installed capital cost figure includes
direct costs only, indirect costs are excluded.
2. The total cost figure applies to 1976/1977 Installa-
tion and does not include escalation factors.
3. The annual operating cost figure is an estimate that
applies to 1977 operations at an 80% unit load factor.
Included In this figure are direct and indirect costs.
4. The S/KW figure is based upon the net generating
capacity of both units (680 MW/unit, 1360 MW total).
5. The cost of one redundant scrubber train is Included
for each system.
1. All cost figures presented are estimates provided
by the utility.
2. The total Installed capital cost figures includes
all direct and Indirect costs plus escalation factors.
3. The cost of the ventuH scrubbers required for par-
ticulate emission control are included.
4. The cost of one redundant scrubbing train is included.
5. The annual operating cost, calculated in mills/kWh, is
based upon a 90* unit capacity factor.
6//Tndir>cX costs are not included in the annual opera-
A&£4Wt*BE:DCo ENVIRONf*
Note: N/A indicates figures are not available.
                                                                          CINCINNATI. OHIO 45346

-------
   APPENDIX A (Continued).   FGD SYSTEM ECONOMICS:   OPERATIONAL SYSTEMS
COMPANY
PLANT
UNITS
TOTAL CAPACITY. HH
Pennsylvania Power
(Continued)
Philadelphia Electric
Eddys ton Generating
Unit No. 1A
316

Tennessee Valley Authority
Widows Creek Steam Plant
No. 8
550




PROCESS
STATUS
START-UP DATE

Magnesium Oxide
Operational
9/75

Limestone
Construction
5/77




REPORTED CAPITAL
COSTS,
S MILLION

20.0

56.284




S/KU

63

102.33




REPORTED OPERATING
COSTS.
J ANNUAL

N/A

5.226 MM




MILLS/KWH

N/A

1.72




CriMMfNTS
7. Operating cost fiq'jre includes maintenance costs.
8. All cost figures arr reported in 1975 and 1977 dollars
1. The total installed capital cost figure is a 1972
estimated value, devoid of any escalation factors.
2. Total direct and indirect costs include the three
first stage paniculate scrubbers and one second
stage SO? absorber. Also included are the SO? re-
covery equipment at the plant, site improvements and
access roads, engineering and contractor's fees and
interest on capital during construction.
3. The costs for the magnesium oxide regenerating
facilities are not included in the total cost figure.
1. The total Installed capital cost figure is an estimate
that includes all e»penditures made by February 1977.
2. Included in the total installed figure are the costs
of the existing ESP and venturi scrubbers for control
of particulate emissions, plus all direct and in-
direct costs, and escalation.
3. Sludge handling and disposal facilities are not
included in the above estimate.
4. The annual operating cost figure is an estimate that
applies to operation in 1977.
5. The annual operating cost estimate Includes partic-
ulate removal costs. Amortization of investment is
not included.
6. The mills/kith figure derived from the operating ex-
penditures is the total annual cost esti»>ates (direct
and indirect) *t a unit capacity fac'pr nf 63*.
Note: N/A Indicates figures are not available.
                                         A-7
                                                                   PEDCo  ENVIRONMENTAL.
                                                                         CINCINNATI. OHIO 45246

-------
A-8
                       PEDCo  ENVIRONMENTAL
                            CINCINNATI, OHIO

-------
           APPENDIX A.   FGD SYSTEM  ECONOMICS:  NONOPERATIONAL SYSTEMS
COMPANY
PLANT
UNITS
TOTAL CAPACITY. MW
Alabama Electric Coop.
Tombigbee Power Station
Nos. 2 S 3
450



Basin Electric Power Coop
Laramie River Station
Nos. 1 and 2
1100

Big Rivers Electric Coop
Reid Stean Station
No. 2
250


Boston Edison Company
Mystic Power Station
!«o. 1
155



PROCESS
STATUS
START-UP DATE
Limestone
Construction
3/78 ft 3/79



Limestone
Contract awarded
4/80 t 10/80

Line
Contract
Awarded
1979


Magnesium Oxide
Terminated
4/72



REPORTED CAPITAL
COSTS,
$ MILLION
40.464



75

16


9.510



t/KU
89.92



68.2

64


63.4



REPORTED OPERATING
COSTS,
$ ANNUAL
240,323








615,000



NILLS/KWH
0.77








3.0



COMMENTS
1. Capital cost figures include upstream participate con-
trol equipment (ESP's).
2. 701 of the flue gas capacity 1s scrubbed.
3. Annual operating costs are calculated for 1978 with a
60" boiler capacity factor.
4. Included in the operating costs are all direct costs
minus malntainence and solid waste disposal costs.
5. Indirect costs are note Included in the operating cost
figure provided.
1. The reported capital cost figure provided in the table
applies to the total installed cost for both double-
loop wet limestone scrubbing systems.
2. The total revenues of the contract awarded to
Research-Cottrel 1 is expected to exceed S35.
3. Breakdown of the capital cost is not available.
1. The reported capital cost figure applies to the amount
of the contract awarded to AAF for a turnkey emission
control installation.
2. The figure includes an AAF-ELEX ESP, two spray towers.
reheater, ancillary equipment, ductwork, and nodular
pre-wired control rooms.
3. All figures are reported In 1976 dollars.
4. Escalation factors, costs, and indirect costs are not
included.
1. All cost figures are reported for the project com-
pletion date of 1974.
2. The total installed capital cost of the Runford cal-
cination facility was approximately S4.5 m.
3. Capital charges are not included because of non-
applicability to a 2-year demonstration program.
4. Operating costs for the acid plant regeneration
facility are not included.
5. Ths^ESJ^of "Bke-up "wqnesium oxide (J150/T) is not
/TiS\ papror-r^ FTMWIRON
No»«: N/A indicates figures are not available.
                                             A-9
                                                                             CINCINNATI. OHIO 45246

-------
  APPENDIX A  (Continued).   FGD  SYSTEM ECONOMICS:   NONOPERATIONAL SYSTEMS
COMPANY
PLANT
UNITS
TOTAL CAPACITY, HW
Boston Edison Company
(Continued)

Central Illinois Light Co.
Duck Creek Power Plant
Ho. 1
400
Central Illinois Public Serv.
Newton Station
No. 1
575

Colorado Ute Electric
Craig Station
Nos. 1 & 2
900




PROCESS
^STATUS
START-UP DATE


Limestone
Operational,
Construction
8/78
Double Alkali

Limestone
Contract
Awarded
Spring, 1979




REPORTED CAPITAL
COSTS,
t MILLION


36
108.5

105




$/KH


90
189

117




REPORTED OPERATING
COSTS.
$ ANNUAL


N/A


15 m




MILLS/KHH





2.7




COMMENTS
6. 3.0 mills/kWh is an estimate for total operation and
maintenance costs, including calcination.
7. BECO and EPA each subsidized approximately SOT of the
costs of the demonstration program. Chemico also
underwrote some of the program costs.
1. The capital cost figure is an estimate of e«pendi-
tures, including $4.0 MH for the ESP, and the cost of
the limestone milling and waste disposal facilities.
2. One module has been completely installed and tempo-
rarily operated from September 1976 to April 1977.
Full system operation is scheduled to commence in
August 1978.
1. The capital cost figure is an estimate covering all
the scrubber unit operation areas.
2. Capital figure is quite high because Of the deliber-
ate overdesign and redundancy incorporated into the
system for achievement of reliable operations.
3. The $/kH figure is calculated on the unit's net
generating capacity of 575 MM. 3T of the unit's net
generating capacity is required to Dower the scrubber
plant.
1. The total capital cost figure is an estimate provided
by the utility that does not include reagent prepara-
tion and sludqe disposal facilities. This figure is
based upon a non-reqenerable SO? scrubbing system
(lime/limestone).
2. The total revenues of the contract awarded to Peabody
Engineered Systems for two limestone slurry spray
tower scrubbing systems is expected to exceed $60 MM.
3. Electrostatic precipitators are included in the
capital cost fiqure.
4. The annual operating cost figure is a preliminary
utility estimate also based upon the installation of
a nonreqenprable 50j scrubbing system.
5. The mills/kWh fiqure is based upon a 70" load factor
Note: N/A indicates figures are not available.
                                          A-10
                                                                   PEDCo  ENVIRONMENTAL
                                                                         CINCINNATI. OHIO

-------
 APPENDIX  A (Continued).  FGD  SYSTEM ECONOMICS:   NONOPERATIONAL SYSTEMS
COMPANY
PLANT
UNITS
TOTAL CAPACITY, MM
Commonwealth Edison
Powerton Station
No. 51
425


Gulf Power
Scholz Steam Plant
Nos. 1 » 2
23
Gulf Power
Scholz Steam Plant
No. 2
20
Illinois Power
Hood River Power Station
No. 4
110


PROCESS
STATUS
START-UP DATE
Limestone
Construction
12/79


Dilute Acid.
Terminated
2/75
Dry Adsorption
Terminated
2/76
Catalytic
Oxidation
Terminated
10/72


REPORTED CAPITAL
COSTS,
1 MILLION
50


3.0
N/A
8.5


$/KW
117.65


130
N/A
82.5


REPORTED OPERATING
COSTS,
$ ANNUAL



N/A
N/A
952.000


MILLS/KWH
8.70


N/A
N/A



COMMENTS
1. The total installed capital cost expenditures apply
to the following timetable: all expenditures will be
made from May 1976 to December 1978; expenditures
of $16 MM will be made from October 1976 to October
1977.
2. The annual operating cost is an estimate which in-
cludes the following items:
0 2.7 mllls/kUh for operation and maintenance.
° 6.0 mills/kWh for auxiliary power requirements.
0 Scrubber life span is estimated for an annual
usage rate of 148,000.000 kWh. This is equivalent
to approximately $900.000 annual for auxiliary
power consumption.
1. The total Installed capital cost figure provided for
the CT-101 prototype unit Includes the scrubbers and
ancillary equipment, engineering costs and contractors
fee. This figure is not representative of a full-
scale application.
1. Actual cost figures for this prototype unit are not
available. Foster Wheeler has published initial
capital cost figures which range from $25 to $35 per
kW for low sulfur removal efficiency and $70 to $75
per kW for high sulfur removal efficiency.
1. Reported capital cost figure represents the total
expenditures during the 2.5 year duration of the
program.
2. The JAW figure is based upon the system's net
generating capacity of 103 NW.
3. ESP cost is included since upstream fly ash removal
is a necessary feature of this regenerate system.
4. The annual cost figure is an estimate representing
system running cosU only. Excluded art capital
charges and a credit for product. This figure trans-
lates into a value of $3.«6 per ton of coal consumed.
Note: N/A Indicates figures are not available.
                                        A-ll
PEDCo ENVIRONMENTAL-
      CINCINNATI. OHIO 45246

-------
 APPENDIX A  (Continued).   FGD  SYSTEM ECONOMICS:   NONOPERATIONAL SYSTEMS
COMPANY
PLANT
UNITS
TOTAL CAPACITY, MM
Indianapolis Power & Light
Petersburg Generating Station
No. 3
530






Kansas City Power ft Light
Hawthorn Power Station
Nos. 3*4
525








Key West Utility
Stock Island Power Plant
37












" PROCESS
STATUS
START-UP DATE
Lines tone
Construction
9/77







Limestone
Injection ft
Net Scrubbing
Terminated
11/72







Limestone
Terminated
10/72












REPORTED CAPITAL
COSTS.
$ MILLION
36.885









5.32











0.750














S/KM
69.9









19











20.7














REPORTED OPERATING
COSTS,
$ ANNUAL





































HHLS/KWH










2.2-2.5











0.7
















COMMENTS
1. Capital cost figure Includes the ESP's Installed
upstream of the scrubber plant for primary particu-
late control ($4.083 MM); scrubbers, pumps, fans.
reheat and all auxiliary equipment ($25.9 MM); sludge
stabilization, fixation, and disposal ($3.5 to $4.0
MM); and total Indirect costs ($1.616 MM).
2. Interest during construction 1s not Included.
3. FGO design and costs are based upon 4.51 sulfur coal.
which 1s the maximum allowable sulfur content for the
scrubber plant.
1. This figure Is unreallstlcally low because these
installations were experimental In nature and were
heavily underwritten by the system supplier.

2. This system has been terminated as limestone-based
system and converted to a wet lime scrubbing system.
The costs of additional slakers, feeders, and other
necessary equipment are not Included.
3. Sludge disposal facilities are not Included In the
total cost figure.
4. The annual operating cost figure does not Include
fixed costs.
1. This system was jointly funded by the EPA and the
utility. The system supplier has also underwritten
a considerable amount of the capital expenditures.
This figure, therefore. Is unreallstlcally low.
2. The utility has had to pay for the cost of a new
primary crushing system.
3. The operating cost figure provided was an original
estimate and has not been corroborated or disputed
by actual experience. This estimate was based upon
the following factors:
t
° Capitalization rate of 101; no taxes, no Insurance.
° Maintenance cost of 5T of equipment cost.
° Labor cost at $20.000 per year.
° Limestone cost at $4.05 per ton.
Note: N/A Indicates figures are not available.
                                         A-12
PEDCo  ENVIRONMENTAL
      CINCINNATI. OHIO

-------
 APPENDIX  A (Continued).   FGD SYSTEM ECONOMICS:   NONOPERATIONAL  SYSTEMS
COMPANY
PLANT
UNITS
TOTAL CAPACITY. MM
Louisville Gas t Electric
Cane Run Power Station
No. 5
183
Louisville Gas ft Electric
Cane Run Power Station
No. 6
277
Minnkota Power Coop.
M.R. Young Station
No. 2
450
Montana Power Co.
Colstrip Plant
Nos. 3*4
Pacific Power t Light
Idaho Power Company
Jin Bridger Plant
No. 3
PROCESS
STATUS
START-UP DATE
Lime
Construction
12/77
Double Alkali
Contract Awarded
2/79
Fly Ash/Line
Construction
8/77
Fly Ash/Lime
Contract
Awarded
7/80 * 7/81
Sodium Carbonate
Contract
Awarded
9/79
REPORTED CAPITAL
COSTS,
$ MILLION
12
16.3
44
N/A
50-60 HH
J/KW
66
58.9
98
N/A
110-120
REPORTED OPERATING
COSTS.
$ ANNUAL

7.3 MM

N/A

MILLS/KWH



N/A

COMMENTS
1. The total installed capital cost is an estimated
figure that includes the costs for Hme handling and
sludge disposal facilities.
1. The total installed capital cost figure is an estimate
provided by the utility.
2. The annual operating cost figure provided is an
estimate for one year's service following the first
three months of opertions. $4.5 million of this total
will be subsidized by the EPA for technology research,
development and report writing. This subsidy will not
be utilized for any capital expenditures.
1. The total installed capital cost figure represents
an estimated value for the unit's entire emission
control system. Including an upstream ESP for pri-
mary participate control ($12 million).
2. The capital cost figure does not include the ex-
tensive sludge handling and disposal strategy proposed
for this unit (vacuum filters and building, conveyor,
by-pass equipment, trucks and front-end loaders.
1. Capital cost figures are currently not available for
publication. The contract recently awarded to the
system supplier is expected to exceed $50 MM for both
units.
1. The total installed. capital cost figures are estimated
values provided by the utility.
2. The system will be comprised of 3 parallel absorp-
tion towers each handling 33.3* of the flue gas
capacity.
3. The reagent, a nominal 30 wt. t Na;C03 purge solu-
tion, will be purchased from a local soda ash
manufacturer.
Note: N/A indicates figures are not available.
                                         A-13
                                                                  PEDCo  ENVIRONMENTAL.
                                                                        CINCINNATI. OHIO 45246

-------
  APPENDIX A  (Continued).   FGD SYSTEM ECONOMICS:  NONOPERATIONAL SYSTEMS
COMPANY
PLANT
UNITS
TOTAL CAPACITY, MM
PotoMc Electric Power
Dlckerson Station
No. 3
190

Public Service of New Mexico
San Juan Station
No*. 1 i 2
715





S«1t River Project
Coronado Station
Nos. 1 t 2
700
South Carolina Public Service
Mlnyah Generating Station
No. 2
280
PROCESS
- STATUS
START-UP DATE
Magnesium Oxide
Terminated
9/73

Hellmn Lord
Construction
11/77





Limestone
Contract
Awarded
4/79 & 4/80
Limestone
Construction
6/77
REPORTED CAPITAL
COSTS,
t MILLION
6.5

89.510





N/A
6.189
S/KW
68

127.87





N/A
24.35
REPORTED OPERATING
COSTS,
t ANNUAL
990,000

7.236 K>





N/A

MILLS/KHH
N/A

5.0





N/A

COMMENTS
1. The total Installed capital cost figure 1s an estimate
provided by the utility in 1973.
2. This figure does not Include regeneration and add
plant costs.
3. The operating cost figure 1s an estimate provided
for 1974 operations. This figure Includes operation
and maintenance costs and acid plant freight and
operation charges. Not included in this figure are
fixed charges, utility charges, project management
and engineering costs.
1. The total Installed capital cost figure is an esti-
mated value that applies to 1977 installation. In-
cluded are all direct and Indirect costs plus an
escalation factor.
2. The J/kW figure Is based on a net generating capacity
of 700 MW.
3. The costs of the venturl scrubbers for participate
removal are Included in the total cost figure.
4. The cost of one redundant scrubber train is Included.
5. The annual operating costs and the mllls/kUh value
derived are estimated for 1978 operations and based
upon a capacity factor of 77%.
6. No credit Is allowed for by-product recovery (this
includes both the elemental sulfur product and the
sodium sulfate purge product for use in pulp and paper
processes.
1. The contracts for the ESP and scrubbing system have
just been recently awarded. Actual capital cost
figures have not yet been determined. The combined
cost of these two new power-generating facilities.
Including emission control, is estimated at 685 MM.
1. Fifty percent of the boiler's flue gas will be
scrubbed for SO? removal. SO? removal efficiency is
69*.
2. The total Installed capital cost figure is an esti-
mated value.
Note: N/A indicates figures are not available.
                                         A-14
                                                                   PEDCo ENVIRONMENTAL
                                                                         CINCINNATI. OHIO 45246

-------
 APPENDIX A (Continued).   FGD SYSTEM ECONOMICS:  NONOPERATIONAL SYSTEMS
COMPANY
PLANT
UNITS
TOTAL CAPACITY. MU
South Carolina Public Service
(Continued)

So. Indiana Gas * Electric
A. 8. Brown Station
No. 1
250


Southern Mississippi Power
R.O. Morrow Generating Plant
Nos. 1 S 2
360

Wisconsin Power ( Light
Columbia Plant
No. 2
527

PROCESS
STATUS
START-UP DATE


Double Alkali
Contract Awarded
4/79


Lilies tone
Construction
11/77 & 6/78

lime/Limestone
Requesting/
Evaluating
Bids
1/80

REPORTED CAPITAL
COSTS,
$ MILLION


8.0


18.847

30

S/KH





52.35

57

REPORTED OPERATING
COSTS,
$ ANNUAL







4.2 MM

MILLS/KWH









COMMENTS
3. Total direct and indirect costs for the ESP provided
for primary participate control upstream of the
scrubbers are included (11. 686 MM).
4. Sludge handling and disposal facilities, utilities
and services costs, interest on capital during con-
struction, and contractor's fees are not included In
the total installed cost figure.
1. FHC was awarded a contract in excess of 18 million
for the design and installation of a double alkali
scrubbing system.
2. Total expenditures for this new plant are estimated
at 1134 MM.
3. Excluded are all other direct and indirect capital
cost factors.
4. The Initial capital Investment and annual! zed costs
are estimated to be 20. to 30 percent and 10 to 15
percent less, respectively, than competing lime and
limestone systems.
1. The total installed capital cost figure is an estimate
that applies to 1975 installation dates.
2. Included in the cost figure are the ESP's. ($5.4 MM
equipment costs for two units), scrubbers and ancil-
lary equipment, fans, construction field expenses,
and Interest during construction.
3. Sludge handling and disposal facilities are not in-
cluded in the total cost figure.
1. The total installed capital cost figure Is a pre-
liminary estimate that includes the scrubbers and
ancillary equipment, erection, disposal piping and
2. Sludge handling and disposal equipment and the up-
stream ESP are not included In this figure.
3. The operating cost figures provided are estimated
values.
Note: N/A indicates figures are not available.
                                         A-15
PEDCo  ENVIRONMENTAL
      CINCINNATI. OHIO 45246

-------
A-16
PEDCo  ENVIRONMENTAL
     CINCINNATI. OHIO -45246

-------
       APPENDIX B

FGD PROCESS FLOW DIAGRAMS
                                PEDCo  ENVIRONMENTAL.
                                      CINCINNATI. OHIO 45246

-------
B-2
PEDCo ENVIRONMENTAL
                          CINCINNATI. OHIO

-------
           I IOUVH

Choila No. 1 FGD System:  General  Flow Diagram.
              B-3
PEDCo  ENVIRONMENTAL.
      CINCINNATI. OHIO 45246

-------
            HIST
            ELIMINATOR
   RILEY
VENTRI-SORBER
  SCRUBBER
LIMESTONE
 SLURRY
t 1
RECYCL
E TANK


PW
                                                               ELECTROSTATIC
                                                               PRECIPITATOR
                                                             VVV
                                         SCRUBBER
                                         I 0 BOOSTER FAN
                                                                   SETTLING POND
                 FLUE GAS
                 FROM
                 BOILER
                                                                                              RECYCLE
                                                                                              TO FGD
                           Simplified  Process Diagram  of the  D
                                                       B-4
eek  No.  1  FGD Module.

   PEDCo   ENVIRONMENTAL
          CI MCI MM ATI. OHIO  -45246

-------
                                                                                              CLEAN GAS
 SERVICE
 WATER
FLUE GAS
             TO BY PASS
              TT  DUCT
 LIME
   Y
 WEIGHT  FEEDER

w
)ER
j '

?L^ 	 ?
LIME SLAKING
AND DILUTION
                                                                           I	     STEAM     I
                                                                         NOT  NE"CE"sS~AR"Y~I?~SufF7ciENT
                                                                           REHEAT GAS IS AVAILABLE
 L-W
  MAKE UP
SLURRY TANK
                                                                                         WASTE
                                                                                        DISPOSAL
                                                                                         SYSTEM
                           Conesville  No. 5  F6D System:   Process Flow  Diagram.
                                                 B-5
                                                                 PEDCo  ENVIRONMENTAL
                                                                         CINCINNATI. OHIO 452.46

-------
Will County No.  1  FGD System:  Gen
                    B-6
ISHfiR ENVIRONMENTAL
      CINCINNATI. OHIO 45246

-------
                              1ST STAGE
                              ADJUSTABLE VENTURI
                              FOR FLY ASH/SO,
                                               S02 ABSORBER SCRUBBER
           RECYCLE RETURN SYSTEHr
                RETURN TO POND
CaS03/S04

FLY ASH SLURRY
            TO
      STABILIZATIQN
        FACILITIES
                         F.  R.  Phillips FGD System:   General  Diagram.
                                        B-7
PEDCo ENVIRONMENTAL
      CINCINNATI. OHIO 45246

-------
                                                                                     LIMESTONE
                                                                                     SILO
                                                                                                     CRYSTALLIZER
THICKENER
         WASTE
         DISPOSAL
WASTE
DISPOSAL
                             Chiyoda Throughbred  101 FGD Prototype:  G
                                    Process Diagram.
                                     PEDCo  ENVIRONMENTAL
                                                                                    CINCINNATI. OHIO

-------
       COAL
       SUPPLY
                                    STACK
                                                   •I.D.  FAN.
                                                           -STACK GAS
                                                           REHEATER
PULVERIZER
RECYCLE
PUMP
                                                                                 CLARIFIER
                                                                                HAKE UP
                                                                                WATER

                                                                            TO ASH DISPOSAL
                                                                            POND
            Terminated Hawthorn  No.  3 F6D  System:  General Process  Diagram.
                                        B-9
                        PEDCo  ENVIRONMENTAL
                               CINCINNATI. OHIO  45246

-------
                    COAL
                    SUPPLY
                                                    STACK
                                                                     .D. FAN.
LIMESTONE
SUPPLY
     FEEDER
                                                                              STACK GAS
                                                                              REHEATER
                                                    STACK GAS "
                                                    SCRUBBER
                                                          RECYCLE
                                                          PUMP
                            Terminated Hawthorn No. 4 FGD System:   G
                                                     E-AO
                                                                                                    CLARIFIER
                                                                                                    MAKE  UP
                                                                                                    WATER
                                                                                               TO ASH DISPOSAL
                                                                                               POND
                                                                                   CINCINNATI. OHIO 45246

-------
                                          STACK
                                                         I.D. FAN
  COAL
  SUPPLY
                                                                    STACK GAS
                                                                    REHEATER
                                        AIR HEATER
                                            DEMISTER
                                         STACK GAS
                                         SCRUBBER
PULVERIZER
                                                 RECYCLE
                                                 PUMP
      Simplified Process Flow Diagram of the Lime Scrubbing
                                            B-ll
                         LIME
                         PREPARATION
                         TANK
                       CLARIFIER
                      MAKE UP
                      WATER

                 TO ASH  DISPOSAL
                 POND
for Hawthorn Units 3 and 4.

PEDCo ENVrRONMENTAL
      CINCINNATI. OHIO 45246

-------
                    ^V(c

La Cygne No.  1 FGD System:  Ge^
      ENVIRONMENTAL
CINCINNATI. OHIO 45246

-------
                                              STACK
COAL SUPPLY-
                                                               I.D.  FAN
    PULVERIZER
STACK GAS

 IR HEATER

    DEMISTER

  MARBLE BED
                                                                      TACK GAS REHEATER
                                     F.D.  FAN
                                                     RECYCLE
                                                     WATER
                                                      STACK
                                                        GAS
                                                     SCRUBBER
                              Simplified Process Flow Diagram of the Terminated
                           Original FGD System Installed at Lawrence.
                                                B-13
                            PEDCo  ENVIRONMENTAL
                                  CINCINNATI. OHIO  45246

-------
      FLUE GAS
ROD SCRUBBER
                00
7
                                                SPRAY TOWER
                                                A
                                       A
                                                A
A
                                     +• EFFLUENT LINE
                                                                    €
                    Lawrence No. 4 Operational  FGD System:   S
                                             B-U
                                               fied Flow Diagram.
                                                  PEDCo  ENVIRONMENTAL
                                                         CINCINNATI. OHIO  45246

-------
          wit n
      WlltR 11
           WCH.
          ctCt«S.
n«'
J r
B(R STACK
irxyir
»T-P»SS
OAWESS
f

^ SCP-JBBCR
1 «ftKir»
                                           FM
                     SPARC
Green  River FGD System:  General  Process Diagram.


                                             PEDCo  ENVIRONMENTAL
                  B-15
CINCINNATI. OHIO 45246

-------
                                                        QUENCHER
           ELECTROSTATIC
           PRECIPITATOR
BOILER
 FLUE
 GAS
                                                                 OEMISTER
                                                                  CONTACTOR
                                                                  SCRUBBFR
                                                                  - MODULE
REACTION
  TANK
DAMPERS -

y

Ql

1
;
                                               QUENCHER
                                                                 -DEHISTER
                                                                CONTACTOR
                                                                 SCRUBBER
                                                                  MODULE
                                                                            ABSOPBER
                                                                             RECYCLE
                                              FAN
              FLOCCULANT
               ADDITION
                  Simplified  Process Flow Diagram  of  the Cane Run No.  4  FGD System.
                                                 B-16
                                                                             PEDCo  ENVIRONMENTAL
                                                                                     CINCINNATI. OHIO  -45246

-------
                                                                          SO 5PM FRESH WATER (AVE )
                                                                         2SOGPM FBESH WATER (MAX.
                                                                                pH 6 OR HIGHER
                                                i.oo
                                               • «.mr CMI/SCIU8MI
«»«• f««««CS Ot»«fSt«T JO'I  ««TIO

   IIOOO CFH
                        dAlfl WATCH

                           «.U>KT
                     CL*»lfltl Dl«ClU*
                                        Paddys Run  No.  6 F6D  System:   P

                                                                B-17
   b  ENVIRONMENTAL
CINCINNATI. OHIO  45246

-------
    MAKE-UP
     LIME
     SLURRY
POND LIQUOR	
   RETURN    f

           TO
         DISPOSAL
          PONDS
  VENTURI/SPRAY
SCRUBBER AND TANK
                        TRAY RECIRCULATION
                               TANK
Montana Power and Light Coldstrip F6D Systems
           General  Process Diagram
                                              PEDCo  ENVIRONMENTAL
                                                    CINCINNATI. OHIO

-------
                                              $*f
                                            17.000 Mffl
473.000 ACm
  3SST
                        S3«m
                        HU1KUM
                                                                           JTEW 763V

                                                                               «W.7 18/Wll

ITPASS
DMPW


1
V
ISOUTICK U9 >r 1
_ OWKR 1 M8.000 XCFM f 119-F 364.480 Ml


'
isounoa
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1300 NT
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LJ UJ nxruRjs
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£€*!
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   KUS
                            Reid  Gardner  FGD Systems, Units 1,  2, and  3:
                                General Process  Diagram.
                                             B-19
PEDCo  ENVIRONMENTAL
       CINCINNATI. OHIO 45246

-------
                                      DISCHARGE
                                      TO STACK
                                                                                     CONDENSER
                                            TRAY TOWER
                                             ABSORBER
            Na2C03
            MAKE-UP
                      PRESCRUBBER
                    (VARIABLE-THROAT
                          VENTURI)
         FLUE  GAS  FROM
            UNIT  #11
FLY ASH PURGE TO POND
furhjftjft^
fimtfL-
y } ^ ^ } ^ ^^

J
* ^
w
^
J-
t
1 '

^
1
/">
J

   TREATED
PURGE STREAM
                            STORAGE
                                BIN
                                    Y
                                    DRIED
                                   SULFATE
                                   PRODUCT
                                                       CENTRIFUGE
                                             SODIUM SULFATE
                                                  CAKE
                   PURGE
                   STREAM
                                                                          TO S02
                                                                         REDUCTION
                                                                           PLANT
               CRYSTALLIZER


           -STEAM
                                                                                         EVAPORATOR/
                                                                                          CRYSTALLIZER
                                  COMPRESSOR
                       NIPSCO D.  H.  Mitchell  No.  11  Wellman Lord/
                                       General  Process  Diagram

                                               B-20
                                  ENVIRONMENTAL
                            CINCINNATI, OHIO 45246

-------
FLUE GAS
   TO
SCRUBBER
                   REHEATER
                     MIST
                   ELIMINATOR
                  OVERFLOW  POTS
                   & MARBLE BED
  RIVER
MAKE-UP
 WATER
                                                            WEIR
                                             THICKENER
                                             UNDERFLOW
                                               PUMP
                                                                     ASH POND
                                                                                     LIMESTONE —i
1 1 	 1

THICKENER





RE

CIS

C
TANK


*x
                                                                                           SLURRY
                                                                                            TANK
                                                                                                  SLURRY
                                                                                                   PUMP
                            ASH POND
                          RETURN PUMP
                     Sherburne No.  1 FGD System:   Simplified  Process Diagram.
                                              B-21
           PEDCo   ENVIRONMENTAL
                  CINCINNATI. OHIO 45246

-------
                                                                               Wl'LK
                                                           riPELINES TO P.EOERVOIR
Bruce Mansfield No. 1 FGD  System:   Simplified  Process Diagram.
                          B-22
PEDCo  ENVIRONMENTAL
       CINCINNATI. OHIO 45246

-------
 FRESH
 WATER	«•
 INLET
    BACKWASH
    SPRAYS
STACK GAS
FROM 1.0.
FANS
 PARTICIPATE
 SCRUBBER
HUMIDIFIED
GAS STREAM
             Mg  (OH), SLURRY
 PARTICULATE
 SCRUBBER
 SURGE TANK
                TO WASTE  WATER
                TREATMENT SYSTEM
                                        tf-MJf.
4f
                                                        CLEAN GAS UUILLl
                                                          MIST ELIMINATORS
                                                         MIST  ENTRAPMENT  SEPARATOR
               S02 SCRUBBER
               SURGE TANK
                                                 O-'--'1
               Eddystone No. 1 FGD System:  Gene

                                   B-23
                                       VENTURI ROD MODULES
                                                                 SCRUBBING  SLURRY  INLET
                                                                      TO Mg S03
                                                                       RECOVERY
                                     PEDCo  ENVIRONMENTAL
                                     S DlagrXtlMCINNATI. OHIO 45246

-------
        I   AIR
        I FUEL OIL>—^REHEATER]—,
             SCRUBBER
I  FLUE GAS
I LIMESTONE
                      A A A
                      T
                     FIRST
                     HOLD
                     TANK
                                CMAKEUP WATER]
                                                I.D.  FAN
SECOND
 HOLD
 TANK
 SAMPLE POINTS

 OGAS COMPOSITION
 ®PARTICIPATE  COMPOSITION & LOADING
 ©SLURRY OR SOLIDS COMPOSITION
                                                                                        i	
        	GAS  STREAM
        	LIQUOR  STREAM
                                                 PROCESS
                                                 WATER
                                                 HOLD
                                                 TANK
                                                                                              STACK
                                                                                      -QlAKEUP WATER|
                                                                              DISCHARGE
                                                             SETTLING POND
                              Shawnee No.  10  Prototype Test Unit:

                                                   B-24
                                          pREQCSagrCJVJVIRONMENTAL
                                                 CINCINNATI, OHIO 45246

-------
         i   AIR   >—	^

         I FUEL OIL >~»| REHEATER"]—-;
IFLUE GAS>-Q-®-
     VENTURI
     SCRUBBER
j   LIME   >-
                                                ®~-fea.D.  FAN
                      SCRUBBER
                      EFFLUENT
                       HOLD
                       TANK
  SAMPLE POINTS
  OGAS COMPOSITION
  ®PARTICULATE  COMPOSITION & LOADING
  ©SLURRY OR SOLIDS COMPOSITION
                                              SETTLING POND
	GAS STREAM
	LIQUOR STREAM
                         Shawnee No. 10 Prototype Test Unit:  General Process Diagram.

                                                                       PEDCo  ENVIRONMENTAL
                                               B-25
                                      CINCINNATI. OHIO 45246

-------
                          FLUE GAS
MAKE-UP WATER
                                                                   VENT  AIR
                                                                    A
                                                      OXIDATION
                                                       TANK
                                                                           CLARIFIED LIQUOR
                                                                                WATER
                 SPRAY TOWER EFFLUENT
                       HOLD TANK
C5
C3
*• »
T




^


!
c
->

— i /W
1 L
i
DESUPERSATURATION
TANK
                                     Shawnee  No. 10 Prototype Test
                         Venturi/Spray Tower  System for 2-Stage Oxid
                             BLEED TO
                           DEWATERING
                          _  SYSTEM
 PEDCo ENVIRONMENTAL
 ..    CINCINNATI. OHIO 45246
sting.

-------
                                    REHEATER
                                        ENTRAPMENT  SEPARATOR
                                                               FLUE GAS DUCT
                                                              FROM POWER HOUSE
                                                       EXISITNG ESP'S
                                VENTURI  CIRCULATION TANKS
                        ABSORBER CIRCULATION TANKS
              ABSORBER CIRCULATION PUMPS
TVA Widows Creek No.  8 FGD Sys
        Schematic Diagram

             B-27
PEDCo  ENVIRONMENTAL
      CINCINNATI. OHIO 4S248

-------
Four Corners Prototype  Scrubber Module:  Cross Section Diagram.
                      B-28
PEDCo  ENVIRONMENTAL
      CINCINNATI. OHIO 45246

-------
BOILER
FLUE-r
GAS
                                                                                               98% GRADE
  SULFURIC ACID
  CONTACT ACID
     PLANT
                             PUMP
                              Mystic No. 6 FGD  System and  Essex Chemical  Plant
                        Regeneration Facility:   Schematic  Flow Diagram.
                                                B-29
PEDCo  ENVIRONMENTAL
       CINCINNATI. OHIO 45246

-------
                                               REHEATER F	1
                                                       n r
 SLURRY
 BLEED
   TO-<-
SETTLING
  POND
              PEABODY/LURGI
              RADIAL VENTURI
•7
                PEABODY
              SPRAYJTOWER
              sb2 "REMOVAL
  PARTICULATE
    REMOVAL
LIMESTONE
                       SLURRY HOLD TANK
                                                              WASHWATER
                                                               RECYCLE
                                                                TANK

                  St.  Clair No.  6 FGD System:   General  Process Diagram.
                                     B-30
                                                             PEDCo  ENVIRONMENTAL
                                                                    CINCINNATI. OHIO 45246

-------
                  SCRUBBED
                     GAS
                                                               SOLIDS
                     VACUUM WATER RECOVERY    H?0
                               U,	--L-
CEA/ADL  Dual  Alkali  Prototype:  General Process  Diagram.
                       B-31
PEDCo  ENVIRONMENTAL

       CINCINNATI. OHIO 45246

-------
2)      ADSORPTION
                                      REGENERATION
             FW-BF Dry Adsorption  Prototype:   Gene
ADSORPTION  SECTION

1.  INLET FLUE
    GAS DUCTING. DILUTION AIR
    DESIGN, AND ADSORPTION
    SECTION OVERALL LAYOUT.
2.  ADSORPTION DISCHARGE FANS.
3.  ADSORBER  DISCHARGE FEEDERS
    CONVEYORS AND SITE GLASSES
    WHICH SHOW CHAR MOVEMENT.
4.  ADSORBER  FEED CONVEYORS.
5.  CHAR BUCKET ELEVATORS.
REGENERATION  SECTION

6.  AIR PREHEATER, SAND
    FLUID BED HEATER, HOT
    SAND BUCKET ELEVATOR.
7.  START UP  AIR HEATER.
8.  SATURATED CHAR SURGE
    TANK, SATURATED CHAR
    FEEDER, REGENERATOR.
9.  SAND HEATER BLOWER.
10. SAND MAKE UP HOPPER,
    FEEDER.
11. HOT SAND  CONVEYOR.
12. CHAR-SAND SEPARATOR
    FEEDER.
13. REGENERATED CHAR
    COOLER.
14. REGENERATED CHAR
    BUCKET  ELEVATOR, CHAR
    MAKE UP HOPPER. FEEDER.
REDUCTION SECTION

15. COAL MAKE UP HOPPER,
    FEEDER  FEED BUCKET
    ELEVATOR.
16. COAL FEED BIN.
17. COAL FEED BIN ACTIVATOR,
    ROTARY  COAL AIRLOCK,
    RESOX  START UP HEATER.
18. RESOX  REACTOR.
19. SULFUR  CONDENSER, TAIL
    GAS BLOWER.
20. CONTROL AIR BLOWER.
21. ASH DISCHARGE FEEDER
22. ASH RECEIVER VESSEL,
    WEIGH  SCALE.
23. SULFUR  STORAGE TANK,
    SULFUR  TRANSFER PUMP.

 PEDCp.  ENVIRONMENTAL

-------
                                                                          CAT-OX MIST
                                                                           ELIMINATOR
  FLUE GAS
FROM EXISTING
    ID FAN
                                                                                          *• STORAGE
                              Wood River No.  4  Catalytic Oxidation FGD System:
                                   Simplified Process Diagram.
                                                B-33
PEDCo  ENVIRONMENTAL
       CINCINNATI. OHIO 45246

-------
                                              STACK
                                                               •I.D.  FAN
COAL SUPPLY-
       FEEDER
    PULVERIZER
STACK GAS

  IR HEATER

    DEMISTER
TACK GAS REHEATER
                                                                                            7   RECYCLE
                                                                                                WATER
                                                      STACK'
                                                        GAS
                                                     SCRUBBER

                             Terminated Operational  FGD  System  at  Lawrence  No. 5.
                                                B-34
                                                                        PEDCo  ENVIRONMENTAL
                                                                              CINCINNATI. OHIO

-------
Stock Island Plant FGD System:  Process Flow Diagram.




                                           PEDCo  ENVIRONMENTAL
                   B-35
                                                 CINCINNATI. OHIO 45246

-------
                                                                       VENTURI
                                                                       SCRUBBER/ABSORBER
                   TO DRY ASH HANDLING SYSTEM
 	/  '  TRANSFE
ASH POND
                          MgO FROM
                         ACID PLANT
MgSO  TO ACID PLANT
                                    Dickerson No.  3 Regenerative FGD System:
                                      General Process Diagram.
                                                  B-36
                                                                             PEDCo  ENVIRONMENTAL
                                                                                   CINCINNATI. OHIO

-------
   ALKALI
STORAGE SILO
       SLURRY 8
      MIX TANK
                                       FLUE GAS FROM
                                       PRECIPITATORS
                                        CONTROL
                                        BUILDING
          MOTOR  CONTROL
  THICKENER  CENTER
OVERFLOW TANK
                        ABSORBE
                        HOLD TANK
 POWER
iPLANT
 STACK
                    ALKALI
                   MIX TANKS
                                          TURBULENT
                                          CONTACT
                                          ABSORBER
                                    Mohave No.  1  Vertical  Test Module:
                                  Simplified Process  Diagram.
                                              B-37
                                                                      PEDCo  ENVIRONMENTAL
                                                                            CINCINNATI. OHIO

-------
                             FOUR SCRUBBER STAGES
                                                                                HOT AIR
                                                                               INJECTION
BOOSTER FAN
MIST ELIMINATOR
               Mohave No. 2 Horizontal Test Module:  Simplified Side View.
                                     B-38
       PEDCo  ENVIRONMENTAL
             CINCINNATI. OHIO 45246

-------
         TO STACK
FLUE  GAS
FROM  VR
BOILER


   HEAT
EXTRACTOR
ASH
                  •MftdtehMMhHJbu^A

                   «» I ^^ | w^
                               REHEATER
                                OEMISTER
                              RECYCLE
                    MARBLE   BED

                      SPRAY
                              •LADDER
                               VANES
                                              WATER
LADDITIVE
             SOLIDS
               TO   -
            DISPOSAL
                   —LIQUID
                                                  CLARIFIER
                         •VACUUM   FILTER
            Simplified Process Flow Diagram of
            Injection and Time-End Scrubbing S
                            B-39
                                                ENVIRONMENTAL
                                           CINCINNATI. OHIO 45246

-------
PEDCo  ENVIRONMENTAL
     CINCINNATI. OHIO

-------
APPENDIX C




DEFINITIONS
                        PEDCo ENVIRONMENTAL.
                             CINCINNATI. OHIO

-------
C-2
PEDCo  ENVIRONMENTAL
     CINCINNATI. OHIO 45246

-------
                                   DEFINITIONS
Boiler Capacity Factor
Boiler Utilization Parameter
Efficiency,
   Particulates
   SO,
FGD Availability Factor
FGD Reliability Factor
FGD Operability Factor
FGD Utilization Factor
FGD Status
   Category 1

   Category 2
   Category 3
 (kWh generation in year)/(maximum continuous generating
capacity in kW x 8760 hr/yr).

Hours boiler operated/hours in period, expressed as a
percentage.
Operational - The actual percentage of particulates re-
moved by the FGD system and the particulate control de-
vices from the untreated flue gas.  All others - The
design efficiency (percentage) of particulate removed by
the FGD system and the particulate control devices.

Operational - The actual percentage of SO2 removed from
the flue gas.  All others - The design efficiency.

Hours the FGD system was available for operation  (whether
operated or not)/hours in period, expressed as a percentage,

Hours the FGD system operated/hours FGD system was called
upon to operate, expressed as a percentage.

Hours the FGD system was operated/boiler operating hours
in period, expressed as a percentage.

Hours FGD system operated/hours in period, expressed as
a percentage.


Operational - Unit has been or is in service removing SO-.

Under Construction - Ground has been broken for installa-
tion of FGD system,  but FGD system has not become opera-
tional.

Planned, Contract Awarded - Contract has been signed for
purchase of FGD system but ground has not been broken
for installation.

                            ^X  PEDCo ENVIRONMENTAL
           -_,           V^^^/       CINCINNATI. OHIO 45246

-------
                                   DEFINITIONS
   Category 4



   Category 5



   Category 6


   Category 7


FGD Vendor


Fuel Characteristics



Identification Number


New



Operational Experience




Process
Planned, Letter of Intent Signed - Letter of intent has
been signed, but legal contract for purchase has not been
awarded.

Planned, Requesting/Evaluating Bids - Bid requests have
been released but no letter of intent or contract has
been issued.

Considering only -FGD Systems - An FGD system is proposed
as a means to meet an SO_ regulation.

Considering an FGD system as well as alternative methods
(Tables 14, 15).

Vendor with a signed contract, letter of intent or strong
commitment because of test unit or past purchases.

Type of fuel, average gross heating value in Btu/lb,
average percent ash and average percent sulfur content
for fuel as fired.

Number of unit in the alphabetical listing in Tables 1,
2, 3 or Tables 14, 15.

FGD unit and boiler were designed at the same time or
space for addition of an FGD unit was reserved when
boiler was constructed.

Operational - Brief summary of FGD system operation
since start-up and description of current month's per-
formance.  All others - Comments regarding state of con-
struction, etc.

Company name if process is patented.  Generic name if
several companies have similar processes.
                                         C-4
                                                             PEDCo ENVIRONMENTAL
                                                                  CINCINNATI. OHIO 4524-6

-------
                                   DEFINITIONS
Regulatory Class
Retrofit


Sludge Disposal



Start-up Date



Unit Cost
A.   New boiler constructed subject to Federal New Source
     Performance Standards.

B.   Existing boiler subject to State Standard that is
     more stringent than the Federal New Source Perform-
     ance Standard (NSPS).

C.   Existing boiler subject to State Standard that is
     equal to or less stringent than NSPS.

D.   Other.

E.   Unknown.

FGD unit must be added to an existing bciler not
specifically designed to accommodate FGD unit.

Comments on disposal method for those units generating
sludge including:  lined or unlined ponds, stabilized or
unstabilized sludge,  and on- or off-site disposal.

Operational - Date when SO2 removal began.  All others -
Date when SO2 removal is scheduled to begin.  Generally
this will be the start-up date of the boiler.

Capital Cost in $/kW including:  S02 absorption and regen-
eration system, S02 recovery system, solids disposal,
site improvements, land, roads, tracks, substation, engi-
neering costs, contractors fee and interest on capital
during construction.

Annualized Cost in mills/kWh including fixed and variable
costs.  Fixed costs include:  interest on capital, deprecia-
tion, insurance, taxes, and labor costs including overhead.
Variable costs include:  raw materials, utilities, and
maintenance.
                                          C-5
                                PEDCo  ENVIRONMENTAL.
                                     CINCINNATI. OHIO 45246

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                                   DEFINITIONS
Unit Location

Unit Name




Unit Rating



Utility Name



Water Make-Up
City and State listed in mailing address.

Unit identification as it appears in Electrical World -
Direction of Electrical Utilities, McGraw-Hill - Current
Edition - or as indicated by utility representative for
installations in planning stages.

Operational - Maximum continuous gross generation capacity
in MW; Preoperational - maximum continuous design genera-
tion capacity in MW.

Name of corporation as it appears in Electrical World -
Directory of Electrical Utilities, McGraw-Hill - Current
Edition - as space permits.

Gallons per minute of make-up water required per MW of
capacity.
                                         C-6
                                                              PEDCo  ENVIRONMENTAL
                                                                   CINCINNATI. OHIO -45246

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