EPA 670/2-73-088
December 1973
                       Environmental Protection Technology Series
  Demonstration  of A Non-Aqueous
  Sewage  Disposal   System
                                Office of Research and Development

                                U.S. Environmental Protection Agency
                                Washington, D.C. 20460

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            RESEARCH REPORTING SERIES
Research reports of the  Office  of  Research  and
Monitoring,  Environmental Protection Agency, have
been grouped into five series.  These  five  broad
categories  were established to facilitate further
development  and  application   of   environmental
technology.   Elimination  of traditional grouping
was  consciously  planned  to  foster   technology
transfer   and  a  maximum  interface  in  related
fields.  The five series are:

   1.  Environmental Health Effects Research
   2.  Environmental Protection Technology
   3.  Ecological Research
   4.  Environmental Monitoring
   5.  Socioeconomic Environmental Studies

This report has been assigned to the ENVIRONMENTAL
PROTECTION   TECHNOLOGY   series.    This   series
describes   research   performed  to  develop  and
demonstrate   instrumentation,    equipment    and
methodology  to  repair  or  prevent environmental
degradation from point and  non-point  sources  of
pollution.  This work provides the new or improved
technology  required for the control and treatment
of pollution sources to meet environmental quality
standards.

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                                             EPA 670/2-73-088
                                             December 1973
              DEMONSTRATION
                   OF A
    NON-AQUEOUS SEWAGE  DISPOSAL SYSTEM
                    by

             Floyd L. Matthew
             Ervin E. Nesheim
             Project  15010 PBK
            Program Element 1BB038
             Project  Officer:

             William  Librizzi
Edison Water Quality Research  Laboratory
         Edison, New  Jersey 08817
               Prepared for:
   OFFICE OF RESEARCH AND DEVELOPMENT
  U.S.  ENVIRONMENTAL PROTECTION AGENCY
         WASHINGTON,  D.C. 20460
    For sale by the Superintendent of Documents, U.S. Government Printing Office
              Washington, D.C. 20402 - Price $1.60

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                   EPA Review .-lotice
This report has been reviewed by the Environmental
Protection Agency and approved for publication.
Approval does not signify that the contents neces-
sarily reflect the views and policies of the Environ
mental Protection Agency, nor does mention of trade
nanes or commercial products constitute endorsement
or recommendation for use.
                           11

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                       ABSTRACT
A prototype non-aqueous wastewatcr treatment systen uti-
lizing recirculated mineral oil as a collection ancl
transport media was installed and operated at the Mount
Rushmore Na'tional Memorial, Rapid City, South Dakota.
The project was conducted to demonstrate the feasibility
and effectiveness of the non-aqueous system for applica-
tion at recreational ancl similarly remote areas.

The non-aqueous system was evaluated for six months
during the 1972 visitation season.  During this period,
data was collected to determine system usage rate and
user waste loading and to evaluate the physical, biological
and chemical content of the flush oil as a function of sys-
tem usage.  System operation and reliability were also
demonstrated during the test period.

The demonstration showed that the non-aqueous treatment
system  is effective in the collection, transport, and
disposal of human waste.  Odors in the oil flush media
and from the treatment system presented an aesthetic
problem which makes the use of this system undesirable
for recreational areas such as Rushmore.  System redesign
to prevent organic accumulations and the routine use of
an oxidizer-bactericide to eliminate odor-producing bac-
terial  activity  is required before this concept can be
suitable  for high-use visible recreational areas.

Water  conservation is achieved when recirculated mineral
oil is  used to collect and transport human wastes.  The
waste  volume is  reduced by 98 percent  in comparison with
conventional water carriage systems.

This  report was  submitted  in fulfillment of Project
Number  15010 FBI: under the partial sponsorship  of the
Environmental Protection Agency.
                           111

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                       CONTENTS


Section                                                  Page

     I   Conclusions                                       1

    II   Recommendations                                   3

   III   Introduction                                      5
             Objectives                                    5
             Scope                                         6

    IV   Aqua-Sans System                                  9
             Flush Fluid Loop                              9
             Waste Disposal System                        14

     V   Incinerator                                      17

    VI   Facilities           .                            19
             Plumbing Modifications                       19
             Electrical Modifications                     21
             Exhaust System Modifications                 21

   VII   Evaluation  Procedures                            23
             Mineral Oil Tests                            23
             Mineral Oil Usage                            24
             Per  Capita Waste Loading                     24
             Public  Acceptance of the Mineral  Oil As
                a  Flush  Fluid                              25
             Maintenance and  Reliability                  26
             Waste Composition                            26

  VIII   Evaluation  Results                               27
         Mechanical  System Performance, Maintenance,
            and  Reliability                                27
             Pump s                                        27
             Reservoir  and Waste Sump                     28
             Waste Sensors                                38
             Oil  Reservoir Cleaning                       38
             System  Vent                                  38
             Miscellaneous                                38
         Oil Maintenance and  Quality                     40
             Suspended  Solids and Water Removal           40
             Bypass  Filter System                         41
             Bacteria Control                             48
             Odor Control                                 48
             Oil  Loss                                     51
             Useful  Life of Mineral  Oil Flush  Fluid      53
             Miscellaneous                                54
                           v

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                        CONTENTS (CONT.)


Section                                                  Page

  VIII   Restroom Facilities                              54
             Flushing                                     54
             Oil Spillage                                 54
             Oil Splashing                                55
             Cleaning                                     55
         Design Criteria                                  56
             Waste Loading                                56
             System Sizing                                59
         Water Conservation                               60
         Summary of Evaluation Results                    60

    IX   Acknowledgments                                  63

     X   References                                       65

    XI   Glossary                                         67


                           APPENDICES

   A     Chrysler Corporation Space Division Technical
           Evaluation of Aqua-Sans Treatment System      A-l

   B     Flush Fluid Specifications                      B-l

   C     Test Procedures                                 C-l
             Coliform Bacteria Counts of Mineral Oil     C-l
             Interfacial Tension of Mineral Oil          C-l

   D     Effect of Flush Fluid on Humans                 D-l

   E     Restroom Cleaning Procedure                     E-l
                                  VI

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                    LIST OF FIGURES


Figure
Number                                                   Page

  1      Aqua-Sans System                                  9

  2      Aqua-Sans System--Block Diagram                  10

  3      Aqua-Sans Reservoir--Sectional View Showing
           Modifications                                  13

  4      Metering Tank and Waste Transfer Valve           16

  5      Visitor Center Restroom Plumbing--Line Diagram   20

  6      Public Acceptance Questionnaire                  25

  7      Cumulative Flush Oil Flow, Water Closet and
           Urinal Flushes, and Waste Collected.
           February 6 Through July 31, 1972               29
                           V Ll

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                         LIST OF TABLES
Table
Number                                                   Page

  1      Aqua-Sans Component List                         11

  2      Oil Flow, Flush Count, and Waste Collection
           Data.   February 6 Through May 15,  1972,
           Operating Period                               30

  3      Oil Flow and Flush Count Data.   June 5
           Through June 9, 1972, Operating Period         32

  4      Oil Flow, Flush Count, and Waste Collection
           Data.   June 28 Through July 5, 1972,
           Operating Period                               33

  5      Oil Flush, Flush Count, and Waste Collection
           Data.   July 6 Through July 31, 1972,
           Operating Period                               34

  6      Hourly Oil Flush Flow Rates.  July 6 Through
           July 31, 1972, Operating Period                36

  7      Determination of Peak to Average Flush Flow
           Ratio                                           39

  8      Primary  Filter/Coalescer Element Replacement
           Record                                         41

  9      Oil Interfacial Tension and Color and Clay
           Filter Changes.  February 6 Through May
           14,  1972, Operating Period                     43

 10      Oil Interfacial Tension and Color.  June 5
           Through June 9, 1972, Operating Period         44

 11      Oil Interfacial Tension and Color and Bypass
           Filter Changes.  June 28 Through July 5,
           1972,  Operating Period                         45

 12      Oil Interfacial Tension and Color and Bypass
           Filter Changes.  July 6 Through July 31,
           1972,  Operating Period                         46

 13      Biocide  Addition Record and Coliform
           Bacteria Test Results                          49
                              Vlll

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                LIST OF TABLES (CONT.)

Table
Number                                                   Page
 14      Results of Public Acceptance Questionnaire       52
 15      Oil Lost with Waste                              53
 16      Restroom Facility Flushes Per User
           Determination                                  57
 17      Waste Collection and Water Closet and Urinal
           Flushes                                        58
 18      Suspended Solids Concentrations of
           Concentrated Human Wastes                      59
 19      Determination of Peak Hourly Flow to Average
           Flow Ratio                                     59
 20      Sump Size, Waste Collection, and Maintenance
           as a Function of Users                         61
                              IX

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                       SECTION I

                      CONCLUSIONS
1.  The prototype wastewater treatment system (Aqua-Sans
system) utilizing recirculated mineral oil can effectively
collect, transport, and concentrate urine and fecal wastes
associated with recreational and remote areas.

2.  Bacterial populations in the mineral oil flush media can
be controlled with commercial biocides.  Bacterial analysis
of oil samples showed that total coliform counts were effec-
tively reduced to zero in most of the samples examined.

3.  Odor problems resulted from inadequate oxidation of the
organic particulate matter which collected in the system
storage reservoir and the primary filter/coalescer.  This
organic matter harbored bacteria which were not controlled by
commercial biocides.  Odors resulted from the accumulation of
organic solids and the associated bacterial growth.  These
odor problems must be eliminated before a mineral oil trans-
port system will be feasible.

4.  The waste sump for separating oil from wastes was improp-
erly designed, and excessive turbulence caused finely divided
organic particulates to carry over into oil storage units.

5.  The mineral oil reservoir contained braces and cross mem-
bers where the solids accumulate.  Braces and cross members
must be eliminated and bottom slopes designed to improve
gravity separation of solids to a central collection point.

6.  A user survey showed that 18 percent of the users ob-
jected to odors around the water closets, and 33 percent ob-
jected to the color of the oil in the water closet bowls.

7.  Attapulgus clay filters and carbon filters used in series
can maintain an interfacial tension above 30 dynes/cm in the
mineral oil, which is required for adequate waste separation.

8.  Water conservation is achieved by using recirculated min-
eral oil to collect and transport human wastes.  The conser-
vation of 240,000 gal. of water at Mount Rushmore during the
demonstration resulted in a reduction in water pumping costs.

9.  The waste volume was reduced by 98 percent in comparison
with conventional water carriage systems, which resulted in
significant reductions in hydraulic loads on the Mount
Rushmore wastewater treatment system.

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10.  Approximately 15 instances of oil overflows from water
closets and urinals resulted in a hazardous condition to users
of the restroom facilities.

11.  The incinerator furnished for the demonstration did not
dispose of the concentrated wastes separated by the Aqua-Sans
system,

12.  The useful life of the mineral oil as a flush fluid
could not be accurately predicted by the results of this
demonstration.  The data does, however, indicate that the
mineral oil can be used as flush media longer than the five-
month operating period conducted at Mount Rushmore.  A proper
filtering system is essential to maintain the oil in a ser-
viceable condition.

13.  Average user waste loading ranged from 0.059 to 0.085
gallons per user.  The ratio of flushes per facility user
was 0.95.

14.  The oil loss with the waste is a function of facility
usage rate and operating level of waste in the waste sump.
During low use periods the oil loss was 3.8 gallons per 1000
gallons waste.  The loss during high use periods was 47 gal-
lons per 1000 gallons waste.

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                         SECTION II

                       RECOMMENDATIONS
1.   Solution of the odor problem will make the Aqua-Sans
system feasible for use in recreational areas where conven-
tional waste disposal methods are impractical or not feasible
or where water conservation must be practiced; however, the
following system design changes are recommended for all
future Aqua-Sans systems.

    a.  Enlarge the waste sump to provide a theoretical
    detention time of 3.5 times the maximum hourly flow.

    b.  Design the inlet to the waste sump to eliminate
    turbulence.

    c.  Time inflows to the waste sump from sensor flushing
    or reservoir pumping to occur during a no-use period.

    d.  Design the flush media reservoir to eliminate sur-
    faces and obstacles that retain solid and liquid wastes.

    e.  Install a dual waste sensing system which requires
    a double failure before oil can be pumped from the
    waste sump.

    f.  Eliminate the vacuum lift system.

    g.  Use an accumulator with a bladder type air chamber.

    h.  Use a metering pump to pump the oil out of the reser-
    voir, through the bypass filter system, and back into
    the reservoir.

    i.  Use a secondary waste holding tank of sufficient
    size to provide waste storage for several hours and
    install equipment to skim the oil from the top of the
    waste to reduce losses.

    j.  Provide a blower in the reservoir vent to provide a
    forced draft on the reservoir.

    k.  Use 4 in. diameter or larger piping for all waste
    piping.  Long radius fittings should be used in all
    piping.

2.  The four bypass filter elements should be changed after
16,000 connected restroom facility uses.

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3.   Biocide addition is dependent on the system usage rate.
Biobor JF must be added in doses equivalent to 185 ppm every
three days for usage rates in excess of 1,000 users per day.

4.   The following studies are also recommended:

    a.  Develop water closet and urinal designs which will
    eliminate splashing and spillage problems.

    b.  Investigate methods for ultimate disposal of concen-
    trated human wastes, which can include the following:

        1.  Incineration;
        2.  Aerobic digestion;
        3.  Anaerobic digestion;
        4.  Soil filters for effluent from 2 and 3 above;
        5.  Irrigation for effluent from.2 and 3 above; and
        6.  Air drying--natural and mechanical.

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                         SECTION III

                        INTRODUCTION
Waste treatment systems which can collect, transport, and dis-
pose of human wastes are needed at remote and recreational
areas where conventional waste disposal methods are impracti-
cal, not feasible, or undesirable, or where water conserva-
tion must be practiced.

The Black Hills Conservancy Sub-District demonstrated the use
of a non-aqueous, recirculating waste treatment system at the
Mount Rushmore National Memorial Visitor Center under the
Environmental Protection Agency grant program.  The Mount
Rushmore National Memorial Visitor Center was selected for
the demonstration because (1) the National Park Service was
agreeable to providing space for the system installation;
(2) the summer visitation to the monument is sufficient to
demonstrate the effectiveness of the system over a wide range
of restroom usage rates; and  (3) the system could be installed
at an existing facility without making extensive permanent
modifications.
OBJECTIVES

The project was conducted with the following objectives:

1.  Demonstrate the feasibility and effectiveness of using a
non-aqueous system for collecting, transporting, and disposing
of human wastes.

2.  Demonstrate that water conservation is achieved by using
a non-aqueous transport fluid.

3.  Determine if the recycled mineral oil can, under variable
load conditions, maintain acceptable physical, biological,
pathological, chemical, and aesthetic characteristics.

4.  Determine the useful life of the mineral oil flush media.

5.  Determine the system operating characteristics as a func-
tion of the per capita waste loading to aid in developing
future design criteria.

6.  Develop operational and maintenance techniques and relia-
bility for the non-aqueous system.

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7.  Determine the effectiveness of incineration as a means of
ultimate disposal of concentrated urine and fecal material.


SCOPE

In 1971 the Black Hills Conservancy Sub-District received an
Environmental Protection Agency grant of $75,213 to demonstrate
an Aqua-Sans system at Mount Rushmore National Memorial, South
Dakota.  The grant, awarded under the provisions of 33 U.S.C.
466 et seq., covered approximately 84 percent of the cost of
the demonstration.  The balance ($14,543) was provided by the
Sub-District.  Eligible costs for the grant included the pur-
chase of the Aqua-Sans system and the incinerator, modification
design and construction at the Visitor Center, system instal-
lation and operation, testing, system removal, and reporting.

The project was conducted in three phases:  (1) Aqua-Sans
system and incinerator design and fabrication; (2) modifica-
tion, construction, and installation at Mount Rushmore; and
(3) test and evaluation.

Chrysler Corporation Space Division designed and fabricated
the Aqua-Sans system, designed the incinerator and contracted
with a vendor for its fabrication, and provided technical sup-
port throughout the project.

The Visitor Center plumbing, electrical, and mechanical sys-
tems were modified during the fall of 1971.  The Aqua-Sans
system and the incinerator were installed in January and
February of 1972.  All system components were placed in the
mechanical equipment room at the Visitor Center.  The system
was connected either to three women's water closets and three
men's water closets and three urinals or to only the six men's
facilities.  The piping necessary for connecting the system
to the toilet facilities was routed through an existing access
tunnel.

The Aqua-Sans system was operated during the period between
February 6, 1972, and July 31, 1972.  Data was collected
during this period to determine the number of facility users,
the amount of mineral oil circulated, the amount of waste
collected, the mineral oil characteristics, restroom user
acceptance, operating and maintenance techniques, and system
reliability.  All work performed under phases two and three
was either under the direction of or by Dakota Engineering
Company, Rapid City, South Dakota.

An incinerator was installed to thermally reduce the concen-
trated human wastes collected in the Aqua-Sans system.  A

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mdcerator pump to divert waste to the existing Mount Rushmore
septic tank and sand filter treatment system was installed as
a backup to the incinerator.

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                       SECTION IV

                    AQUA-SANS SYSTEM
 The Aqua-Sans system,  pictured in Figure 1,  is a non-aqueous
 sewage  disposal system developed by the Space Division of the
 Chrysler Corporation (CCSD) .   This system, which utilizes
 recirculated mineral oil  as  the transport fluid, is  shown
 schematically in Figure 2, while Table  1 presents a  descrip-
 tive listing of the  system's  major components.   A detailed
 description of the system and its operation  is contained  in
 Appendix A, Chrysler Corporation Space  Division Technical
 Evaluation of Aqua-Sans System.   Appendix B  lists the  tech-
 nical specifications for  the  mineral  oil, Sontex 60T.
              Figure 1. Aqua-Sans System


The Aqua Sans system consists of two sub-systems
fluid loop and waste disposal system.
flush
FLUSH FLUID LOOP
Mineral oil flow is dependent on the toilet facility usage
and the flow rate through the bypass filter system.

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     VAC.
     PUMP
      10
                 METER-
                   ING
                  TANK
 to -5,
sewer
     MAC.
     PUMP
         incinerator
      CONTROL VALVE
  O  FLOW SELECTSR

      BLOCK VALVE
      AIR

      WASTE

      OIL

      FLOW DIRECTION
RESERVOIR f"
                                       r-"-—,
                                         WASTE
                                          SUMP
from toilets
                                                                             •—••to toilets
                      BYPASS
                      FILTER
                      SYSTEM
                       ACCUMU-
                        LATOR
                    RECIR.
                    PUMP

                        FLOWMETEFfl
                PRIMARY
                 PUMP
          PRIMARY
          FILTER
            NUMBERS  KEYED TO  TABLE I .
                          Figure  2.  Aqua-Sans System--Block Diagram

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                        Table 1. Aqua-Sans Component List
Fig.  2
Number

   1

   2

   3
   4

   5
   7

   8


   9

  10

  11


  12
      Component

Primary Pump

Primary Flowmeter

Primary Filter/
 Coalescer
Primary Filter
 Elements

Accumulator

Clay Filter Housing
Clay Filter Elements

Carbon Filter Housing
Carbon Filter Elements

Sediment Pump

Waste Sensor


Waste Overfill Sensor

Vacuum Pump

Waste Transfer Seal
 Valve

Macerator Pump
       Description

2V x 2" Mod # C2116130

IV Mod # 1725C
4" x 4" Mod # V1633-B2
# 1-6330
# SO-436-V

82 gal. with separator
IV x Ik" Mod # VC-818
# CO-718CC
# 6436227

1200 gph Mod # 390 2690

Electr-0-Probe
Mod # B-07-SS

Same as 8

3/8" Mod # 1022-V-2-G272X


3" flexible valve

1--1V x 1" Mod # 406-M-l
2--4" x IV Mod # SPG-150
      Manufacturer

Flint e. Walling, Inc.

Badger Meter, Inc.
Velcon Filters, Inc.
Velcon Filters, Inc.
Velcon Filters, Inc.

Flint 5 Walling, Inc.

Velcon Filters, Inc.
Velcon Filters, Inc.

Puritan Industries, Inc.
Puritan Industries, Inc.

Sears

CE In-Val-Co Combustion
Engineering, Inc.

Same as 8

Cast Manufacturing Corp.
Flexible Valve Company

Oberdorfer Pump Division
Hydr-0-Matic Pump Co.

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Primary Flow

Upon demand, resulting from the flushing of a connected
toilet, mineral oil from the accumulator was delivered to
flush the wastes from the toilet and transport these wastes
to the Aqua-Sans system through a 4 in. diameter sewer pipe.

The oil-waste mixture entered the top of the waste sump
through a vertical inlet and passed through an 8 in. air gap
before meeting the oil surface in the waste sump.  Here the
waste, with a specific gravity close to 1.0, settled, while
the oil (specific gravity 0.83) overflowed into the storage
reservoir for treatment and reuse in subsequent flushes.
Settled wastes collected in the bottom of the sump for
transport to the incinerator for ultimate disposal.

The oil storage reservoir had a maximum oil storage of 250
gal., and the waste sump 100 gal. above the oil-waste inter-
face.  The total oil volume in the system, including storage
in the accumulator, pipes, and filters, was 360 gal.  The
reservoir and waste sump were sized to provide a 10-minute
theoretical detention time at a flow rate of 30 gpm.

Initially the oil, prior to overflowing into the storage
reservoir, was passed through a cone screen for preventing
large solids carryover.  The oil was then passed through a
horsehair-fiberglass gross coalescer (which was placed hori-
zontally in the reservoir) for removing water from the oil.
During the demonstration period  (see Section VIII, Reservoir
and Waste Sump), the cone screen was replaced with a cone-
shaped horsehair-fiberglass coalescer.  A bag filter was
also installed at the top of the sump, and the horsehair-
fiberglass gross coalescer removed.  Figure 3 shows a sec-
tional view of the reservoir and the modifications which
were performed.

The primary pump delivered oil from the storage reservoir
through the accumulative flow meter and primary filter to the
accumulator and maintained the pressure in the accumulator
between 30 and 50 psig.

The primary filter contained three cloth-covered filter ele-
ments for coalescing water and removing waste particles
larger than 20 microns from the oil.

A small recirculating pump was provided to pump oil and
water from the low end of the reservoir to the waste sump.
                               12

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              AS  RECEIVED
              AFTER MODIFYING
              I-CONE SCREEN REMOVED
               GROSS COALESCER INSTALLED
              2-GROSS COALESCER REMOVED
              3-BAG FILTER INSTALLED
             Figure  3.   Aqua-Sans Reservoir
  Sectional View  Showing Modifications (Not to Scale)

Bypass Flow

A bypass filter system  containing one attapulgus clay filter
was supplied with the system for removing color, dissolved
contaminants,  and finely divided suspended solids from the
oil.  After several  modifications, the bypass filter system
consisted of two  attapulgus clay filters, one dual element
carbon filter, and a rotometer-type flow rate indicator.
The filters were  arranged with the clay filters in parallel
with the dual-element carbon filter in series and downstream
of the clay filters.  Each clay filter was rated at 1 gpm
                           13

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and the carbon filter was rated for 2 gpm.  Manual control
valves were used to control the oil flow through the bypass
filters (see Figure 2).
WASTE DISPOSAL SYSTEM

The waste separates from the mineral oil and settles to the
bottom of and is stored in the sump for later disposal.  Two
capacitance-type sensors detect the oil-waste interface as
it rises in the waste sump; one is located at the 12 gal.
level and the other at the 35 gal. level.

When approximately 12 gal. of waste is collected in the sump,
the lower waste sensor is actuated, causing the waste trans-
fer valve to close and the vacuum pump to operate.  The
vacuum pump produces a vacuum in the metering tank, which
causes the waste in the waste sump to flow to the metering
tank.  A float switch in the metering tank shuts the vacuum
pump off when approximately 10 gal. of waste has entered the
metering tank.

The waste flow from the metering tank depends on the method
of disposal being used in conjunction with the Aqua-Sans
system.
Incinerator

The Aqua-Sans system was designed for automatic operation
with the primary method of waste disposal being incineration.
In the "incinerator mode," the waste was delivered by gravity
to the incinerator through a 3 in. diameter sewer line.
Approximately one hour was required to burn the waste.  Fol-
lowing the dump to the incinerator:

     (1) the recirculating (sediment) pump came on for approxi-
     mately 5 seconds to pump any liquid waste in the low end
     of the reservoir to the waste sump;

     (2) the sensor flush selenoid valve opened and allowed
     oil from the high pressure system to spray past the two
     waste sensor probes to remove any waste which may have
     collected on the probes; and

     (3) the water flush valve opened, allowing water to spray
     into the metering tank and over the cone screen in the
     sump.  The water flush was removed at the same time the
     cone screen was removed.
                               14

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The waste overfill sensor (upper sensor) actuates when
approximately 35 gal. of waste has accumulated in the sump.
This actuation causes the operating mode to automatically
switch to the "sewer mode."  The waste in this mode was
transferred from the metering tank through a macerator pump
to the Mount Rushmore sewer system.


Backup Disposal

Because of incinerator failure (see Section V), the primary
mode of operation used during the demonstration period was
"sewer mode."

The system was supplied with an Oberdorfer macerator pump
with a 1% in. inlet and a 1 in. outlet.  This pump was
designed to pump wastes from the waste sump to the Mount
Rushmore system when the incinerator was not operating or
waste was collecting at a faster rate than the incinerator
burn rate.  Tests performed with water in the sump indicated
that the 1% in. pump could pass sanitary napkins.  Similar
tests with plastic covered disposable diapers plugged the
2 in. waste pipe connected to the 1% in. pump inlet.  Inlet
modifications did not eliminate the problem.  The Oberdorfer
macerator pump was replaced with a larger pump in June, 1972,

A new macerator pump, manufactured by Hydr-0-Matic Pump
Company, was installed downstream from the waste transfer
valve.  The metering tank with a blind flange installed on
the downstream side of the. waste transfer valve is shown in
Figure 4.  The new macerator was connected where the blind
flange is shown in Figure 4.  The waste transfer valve was
left in place to isolate the macerator pump if maintenance
was required or plugging occurred.

Several alarms were installed in the control system.  The
waste overfill sensor actuated a waste overfill alarm.  If
the automatic cycle operated properly, the alarm cleared
approximately 2 minutes after the waste level dropped below
the sensor.  A tank overfill and a long dump alarm were also
provided on the metering tank.
                             15

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      - »





               Figure 4.
Metering Tank and Waste Transfer Valve
                  16

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                       SECTION V

                      INCINERATOR


A two-stage incinerator, designed to burn 10 gal. of concen-
trated human waste per hour, was furnished with the Aqua-Sans
system as the primary method of disposing of the waste col-
lected in the Aqua-Sans system.

Incinerator draft problems were encountered during the check-
out of the incinerator in February, 1972, so no burns were
made in the automatic mode.  During the months of February,
March, and April, approximately 25 trial burns were conducted,
with water added to the burn pot, while trying to obtain a
draft on the incinerator.  A draft inducer was installed in
March, which resulted in a marginal draft condition during
portions of an operating period.

In April it was observed that  the insulation in the primary
chamber was starting to flake  off.  .At about this same time,
the  insulation in a similar incinerator being tested for the
Navy failed because of flaking.  Apparently the unoxidized
gases caused a thin layer of the exposed insulation to "flux"
(become hard), flake off, and  expose a new layer of insula-
tion.  During disassembly of the incinerator, it was found
that the insulation in the  secondary chamber was exhibiting
the  same deterioration as that in the primary chamber.

Approximately six complete  waste burns were conducted in
addition to the trial burns.   No data was collected on the
residue  (ash) remaining after  a burn.

The  incinerator operation was  discontinued because of the
design problems and the time factor  involved for modifying
the  incinerator; and all collected wastes were pumped to the
Mount Rushmore sewer system.
                           17

-------
                      SECTION VI

                      FACILITIES
The Visitor Center plumbing, electrical, and mechanical sys-
tems were modified to accept the Aqua-Sans system and the
incinerator.  Details regarding the modifications are pre-
sented below.
PLUMBING MODIFICATIONS

Connected Facilities

As shown in Figure 5, the six water closets, numbers W1-W3
and M1-M3, and the three urinals, numbers U1-U3, were con-
nected to the Aqua-Sans unit.  A valve header was installed
to enable valve control of either the backup water supply or
the Aqua-Sans system to either the three connected women's
water closets, the three connected men's water closets and
urinals, or all nine connected facilities.

Three-port, ballcentric valves were placed between W3 and W4
and also between M3 and M4.  Ball valves were placed in the
urinal drain pipes.  These valves could be positioned in the
drain to the Aqua-Sans system when oil was to be used as a
flush fluid and to the Mount Rushmore system when water was
to be used.

The waste and supply pipes for the water closets were located
in a 2-foot wide divider room between the men's and women's
restrooms.  The piping to the urinals was located in a 5-foot
high crawl space under the men's restroom.  Access to the
divider room was through an access tunnel from the furnace
room.
Material Compatibility

The use of mineral oil as a flush fluid requires that special
attention be given to materials used for pipes and valves.
The "Royal" flushometer valves built by Sloan Valve Company
were replaced by Sloan's "Naval" valves, which were modified
to eliminate materials not compatible with mineral oil.
Flush  Counts

Flow switches were  installed  in  the  individual supply pipe to
each of  the six  connected water  closets.  Each flow switch was
                          19

-------
from lavs
— * 1l -*- from

WOMEN A MFM |QV» WOMFM MFM





















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>

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J


J



i «H J i


— i • .


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H

j
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1
< r- _ W6Q
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3

< ^ ONFLOW SWITCHES W4Q
\ /-^FLUSHOMETER
< \ ° VALVES W3Q
^— QFLOW METER
< -^FLOW DIRECTION W2f\
>— —TUNNEL W
-C V-l —PIPE w,
to fountain

and lavs

r | 	 1
-J l" FROM
,^-~

•MB,

	 MMtitKMlUK

	 ^4 TO WATER 2i~
AQUA-SANS (POTABLE) Z

c
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H ta



-6,
4
^









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•





/

I1
dh
dh
^

..
»•
QM6
OM5

QM4 \v
QM3 \
U3O
OM2 u2(>
Ow uiCH
1 to fountain
— and lavs
j — •



^~»
i
	 -OIL 2^"

—WATER 2"
(NON POTABLE)














WASTE PIPING WATER ANO OIL SUPPLY PIPING
Figure 5. Visitor Center Restroon Plumbing--Line Diagram.

-------
connected to an electromechanical counter.  Flush fluid through
the supply pipe to a water closet caused electrical  contacts
in the flow switch to close, which in turn caused the connected
counter to register one count.

The total oil flow to the urinals was recorded by a  cumulative
flow meter placed in the urinal supply pipe.
ELECTRICAL MODIFICATIONS

Electrical power requirements for the Aqua-Sans were two 50-
ampere, 115 VAC circuits.  The incinerator required a 30-
ampere, 115 VAC circuit.  Three separate power receptacles
were installed to provide power to the Aqua-Sans system and
the incinerator.
EXHAUST SYSTEM MODIFICATIONS

The incinerator exhaust pipe was an 8 in. pipe capable of
withstanding temperatures up to 700°F.

The chimney at the Visitor Center is constructed of stone
with a 16 x 21 in. clay tile liner rated for 2000°F.  An
adapter was constructed and installed to connect both the
incinerator exhaust pipe and the furnace exhaust pipe into
the chimney.
                           21

-------
                      SECTION VII

                 EVALUATION PROCEDURES
The following procedures were employed during the demonstra-
tion period.
MINERAL OIL TESTS

Bacteria Counts

The laboratory procedure for determining coliform bacteria
counts is listed in Appendix C.  The listed procedure is a
modification to the Eos in Methylene Blue (EMB) presumptive
test for coliform bacteria outlined in "Standard Methods for
the Examination of Water and Wastewater.Md)  The results of
the tests were used to determine dose requirements and to
evaluate the effectiveness of biocides.

Exact colony counts were not obtained since the goal was to
maintain a zero bacteria count in the oil.
Interfacial Tension

The interfacial tension (IFT) of the Sontex 60T mineral oil
was used as an indication of the effectiveness of the filter
systems in removing oil contaminants.

Initially, IFT was determined using the oil rise on filter
paper strips, as outlined in Appendix C-2-1.  The oil rise
method was found to be both inaccurate and impractical, how-
ever; so an Interfacial Tensiometer was obtained for IFT
determination.  The standard method listed in ASTM:D971-50,
"Interfacial Tension of Oil Against Water by the Ring
Method,"(2) was used for all IFT measurements made after June
1, 1972.  Appendix C-2-2 discusses ASTM:D971-50.
Color

The color of the mineral oil was determined using an Alpha-
Platinum-Cobalt scale color comparitor.  The color scale used
on the "Hach" color comparitor ranged from 0 to 100 color
units.  Tap water was used as the comparison fluid, with
unused Sontex 60T having a color of 0 units.
                            23

-------
MINERAL OIL USAGE

Usage Rates

The totalizing flow meter located downstream from the primary
pump in the oil supply pipe was read at various intervals to
establish average and peak oil usage rates.


Oil Loss

Oil loss was attributed to (1) leaks in the piping; (2) oil
retained in filters after filter replacement; (3) oil spillage
including spillage while handling and resulting -from occasion-
al overflow of urinals or water closets; (4) oil lost from
testing; and (5) oil carryover with the waste.  The oil lost
with the waste was of greatest concern since the waste was
being pumped to the Mount Rushmore septic tank-sand filter
treatment plant.  It was not possible to measure the total
oil lost with the waste.  The average oil lost per waste dump
was determined for several different time intervals by calcu-
lating oil balances for the periods when it was possible to
account for all oil added to or lost from the system.


PER CAPITA WASTE LOADING

The determination of the per capita waste loading required
data on the number of connected facility users and the
amount of waste collected from these users.
Restroom Users

A method of counting the number of connected facility users
which was not subject to vandalism by the users was needed.
The number of flushes for the six connected water closets
was counted separately and the total oil flow to the three
urinals was recorded.  User counts were made during several
time intervals and the ratio of the number of flushes per
user was determined to provide a conversion factor for deter
mining the number of users from the flush counts.
Waste Collected

Electromechanical counters were used to record the number of
waste dumps to the incinerator and to the sewer.
                               24

-------
 The amount of waste per dump was determined to be 10.5  gal.
 -  .2 gal. prior  to  the start of the  demonstration period.

 The per capita waste loading (gallons  per day per person)  was
 determined by dividing the waste collected (gal.) over  a  time
 interval by the  number of connected  facility users during  that
 time period to give gal.  waste per person.  It should be noted
 that there are several restrooms at  Mount Rushmore, so  no  cor-
 relation is made for waste per monument visitor.


 PUBLIC ACCEPTANCE OF THE MINERAL OIL AS A FLUSH FLUID

 A  survey was conducted in which the  restroom users were asked
 to fill out the  questionnaire shown  in Figure 6.  The ques-
 tionnaires were  distributed in the men's restroom after the
 women's facilities  were disconnected from the Aqua-Sans sys-
 tem.  Boxes with the questionnaires  were hung near the  three
 urinals and the  three water closets  for specified periods  of
 time,  which were usually two hours.  The number of flushes
 were recorded for that time period and the questionnaire
 return rate per  user was determined.
     NGN-AQUEOUS SEWAGE DISPOSAL SYSTEM DEMONSTRATION PROJECT

The  toilet facility you just used is connected to a closed-loop sewage
disposal system which  uses oil instead of water for a flush fluid.
You  can assist in the  evaluation of the system by completing this card
and  dropping  it in the box at the restroom exit.

                                Satisfactory    Not Satisfactory

Flush fluid color                    D

Odor                               D

General appearance and operation       I	I             LJ

Comments:	
this  project is sponsored in part by the Environmental Protection
Agency, the National  Park Service, and the Black Hills Conservancy
Sub-District.
        Figure 6. Public Acceptance Questionnaire


                            25

-------
The questionnaire shown in Figure 6 was used to determine the
public acceptance of the use of a non-aqueous flush fluid
which differed in appearance from water and occasionally pro-
duced odors not usually present in restrooms.  Specific items
included in the questionnaire were (1) flush fluid color,
(2) odor, and (3) general appearance and operation.  A section
was also provided for comments.
MAINTENANCE AND RELIABILITY

Complete records in the form of a log book were kept during
the demonstration on system reliability, maintenance require
ments, down time, and repairs.
WASTE COMPOSITION

Concentrated waste samples were collected from the 1 in.
waste pipe to the sewer.  Each sample was analyzed for total
suspended solid? and volatile solids in accordance with Stan
dard Methods.t1-
                               26

-------
                     SECTION VIII

                  EVALUATION RESULTS
The Aqua-Sans system was operated between February 8, 1972,
and July 31, 1972, with two shutdown periods, May 15 through
June 8 (to obtain restroom attendants) and June 10 through
June 27 (to replace macerator pump).  During this period,
the system was evaluated using the evaluation procedures
explained in Section VII.  The system evaluation results are
presented under the following subheadings:   (1) Mechanical
System Performance, Maintenance, and Reliability; (2) Oil
Maintenance and Quality; (3) Restroom Facilities; (4) Design
Criteria; and (5) Water Conservation.  Appendix A provides
the CCSD review and analysis of test data from the system
evaluation.
MECHANICAL SYSTEM PERFORMANCE, MAINTENANCE, AND RELIABILITY

Pumps

(a) Primary Pump.  A total of 548,850 gal. of oil were cir-
culated during the operating period.  Soon after start of
the operating period, the shaft seal began to leak a few
drops of oil a day.  The leak remained constant during the
demonstration period, and no maintenance was required.  No
other problems were encountered with the primary pump.

(b) Vacuum Pump.  The Cast vacuum pump was required to vacuum
lift the waste from the sump into the metering tank.  The
average operating time was 10.5 seconds.  The pump was sup-
plied with a wick type oiler which was designed for longer
operating periods.  As a result of improper lubrication,
vane sticking problems caused vacuum pump failure on three
different occasions during the last two weeks of operation.
Field repairs, which consisted of pump dismantling, clean-
ing, and reassembling, were performed after each failure.

(c) Macerator Pump.  The system was supplied with an Oberdorfer
macerator pump with a 1% in. inlet and a 1 in. outlet.  The
small inlet resulted in plugging problems; and during the
June shutdown, the Oberdorfer macerator pump was replaced
with a 1% hp. Hydr-0-Matic macerator pump which had a 4 in.
inlet and a lh in. outlet.  During the June 28-July 31, 1972,
operating period, the Hydr-0-Matic macerator pump trans-
ported approximately 3,300 gal. of waste with no pump mal-
functions.
                          27

-------
Reservoir and Waste Sump

A brown, flocculent residue of finely divided particulate
matter began to accumulate in the oil reservoir after two
weeks of operation.  The residue also collected on the cone
screen in the waste sump and on the horizontal gross coalescer,
Turbulence at the entrance to the waste sump was the primary
cause of this waste carryover.  In addition, operation of the
recirculation pump and the sensor flush contributed to this
problem.  The cone screen and the gross coalescer were removed
May 14, 1972, and a smaller coalescer was installed in place
of the cone screen..  Removal of the gross coalescer eliminated
a large collection area for the waste; however, the internal
cross braces and the inadequately sloped reservoir bottom con-
tinued to provide collection surfaces and traps for the par-
ticulate matter.

Cumulative flush oil flow, facility flushes, and waste collec-
tion are shown in Figure 7.  Interval oil flow, flush count,
and waste collection data are presented in Tables 2 through
5.  Data were collected at one- to four-day intervals for
February 6 through May 15, 1972, and at daily intervals for
the remainder of the operation.  Hourly data were collected
for oil flow and flush counts between July 6 and July 31,
1972, when the Aqua-Sans unit was connected to only the men's
restroom.  Hourly flush oil flow data are presented in Table
6.

The maximum facility usage occurred between 2130 hours on
July 2 and 2130 hours on July 3, 1972, with 9300 gal. of flush
oil being recirculated.  During this period, a total oil flow
of 11,120 gal. was recorded.  During the 19-hour period when
the restrooms were open for use, the six water closets and
three urinals were flushed a total of 1766 and 1178 times,
respectively, with an average flush flow of 485 gph.  This
flow demand and similar high demands for the June 28 through
July 5, 1972, period (Table 4) resulted in insufficient oil
detention time; and as a result, the water content of the oil
was above saturation during portions of this period (see page
43).

The three women's water closets were switched to water flush
the morning of July 6, 1972, leaving only the six men's
facilities connected to the Aqua-Sans system.  The peak
daily usage occurred July 26, ,1972, with 3260 gal, of oil
being used for 546 water closet and 1227 urinal flushes,
with an average flush flow of 172 gph.  The peak hourly flush
flow on July 26 was 378 gal.  As shown in Table 6, peak
hourly flows exceeded 300 gal. 18 times between July 6 and
July 31, 1972, with the peak hourly demand of 385 gph occur-
ring July 30, 1972.

                               28

-------
    O
    o
    §"
    o
    8
    Q,
    o-J
o
8
in
           o
           iro
          UJ
           CM
           o-1
O
O
                  CM
                  8
                  §1
     §
    •d
          —flush oil
          —waste
          •—flushes
                      6 12 18 24
                     FEBRUARY
                     6 12 18 24
                       MARCH
                          6 12 18 24
                           APRIL
6 12 18 24
   MAY
6 12 18 24
  JUNE
6 12 18 24
  JULY
Figure  7.  Cumulative Flush  Oil Flow,  Water Closet  and Urinal Flushes,  and Waste
               Collection.   February 6 Through July 31, 1972

-------
      Table  2. Oil Flow, Flush Count,
      May  15,  1972, Operating Period.
                                and Waste Collection Data.  February 6, 1972, Through
O-)
o
Date

 2/6
2/10
2/13
2/15
2/19
2/21
2/25
2/28

 3/1
 3/3
 3/6
3/10
3/13
3/15
3/17
3/20
3/24
3/27
3/28
3/31

 4/3
 4/7
4/10
4/14
4/17
4/21
Time

1430
0630
1500
0600
1445
0830
1000
1000

0745
0700
0715
0645
0700
0700
06-30
0630
0630
0700
1730
1400

0715
0730
0645
0930
0700
0700
                             Interval Oil
                             Flow  (Gal.)
                          Total   Flushing
0
7 ,.300
7,540
4,255
5,460
6,390
8,210
4,500
3,130
2,685
4,000
6,075
5,940
3,355
3,930
6,700
6,470
6,235
3,920
6,730
7,960
9,350
6,790
8,820
6,585
5,415
0
200
495
155
610
950
495
645
200
115
570
520
890
220
275
1405
775
1190
640
990
1885
1360
1460
980
1575
805
  Interval
Water Closet
   Flushes

      0
     29
     77
     25
    102
    160
     91
    108

     31
     17
     94
     96
    144
     35
     44
    231
    131
    201
    105
    165

    318
    231
    244
    158
    263
    130
Interval
 Urinal
 Flushes

     0
    59
   143
    32
   116
   175
    43
   117

    26
    33
   108
    42
   185
    48
    37
   234
   178
   206
   129
   183

   325
   226
   268
   210
   302
   171
Interval
  Waste
  (Gal.)

  .0
 8.5
10.5
10.5
10.5
16.5
12.5
18.0

 4.0
 2.0
20.0
 3.5
27.5
 7.0
 7.5
44.0
15.0
31.5
17.0
25.0

47.0 (est)
33.0 (est)
37.0
37.5
38.0
24.0 (est)

-------
                              Table 2. (Cont.)
Date

4/24
4/28

 5/1
 5/5
 5/8
5/12
5/14
Time
  Interval Oil
  Flow (Gal.)
Total  Flushing
0630
0700
0730
0700
0630
0745
2230
5,635
5,955
8,125
9,270
6,010
8,310
10,980
1745
1095
2165
1105
19-00
1855
3175
  Interval
Water Closet
   Flushes

    299
    177

    379
    180
    326
    315
    549
Interval
 Urinal
 Flushes

   276
   218

   297
   116
   298
   286
   460
Interval
  Waste
 (Gal.)

  49.5
  29.0

  59.0
  39.0
  42.0
  49.0
  73.0
Note:  Three women's and six men's restroom facilities connected to Aqua-Sans.

       Example of Interval data:   Interval oil flow--7300 gal.  total oil flow
       between 1430 hrs on 2/6 and 0630 hrs on 2/10.

-------
Table 3. Oil Flow and Flush Count Data.
Operating Period.
                             June 5, 1972, Through June 9, 1972,
Date

 6/5

 6/6

 6/7
 6/8

 6/9
Time

0915
1400
0600
1530
1420
0500
1400
0530
1400
2000
  Interval Oil
  Flow (Gal.)
Total  Flushing
0
2,153
4,865
4,514
6,501
3,954
4,356
4,753
4,691
1,994
0
1430
2880
3445
3495
1910
1665
1780
2325
1155
  Interval
Water Closet
   Flushes

      0
    248
    502
    593
    600
    322
    273
    302
    402
    197
Interval
 Urinal
 Flushes

     0
   191
   369
   480
   495
   300
   299
   267
   315
   169
Note:  Three women's and six men's restroom facilities connected to the Aqua-Sans
       Example of Interval data:  Interval oil flow--2153 gal. total oil flow
       between 0915 and 1400 hrs on 6/5.

-------
Table 4. Oil Flow, Flush Count,
July 5, 1972, Operating Period.
                         and Waste Collection Data.  June 28, 1972, Through
                      Interval Oil
                      Flow  (Gal.)
Date
6/28

6/29

6/30

7/1
7/2

7/3

7/4

7/5

7/6
Time
0530
1650
0800
2030
0530
1745
1400
0615
2130
1645
2130
0600
2130
1400
2130
0530
Total
0
6645
3436
7778
1830
5539
5978
5626
9225
9131
1989
1346
10859
5926
4586
1063
Flushi
0
5855
1710
6090
195
4575
3905
3410
8335
7740
1560
120
7930
4885
3815
205
                                    Interval
                                  Water Closet
                                     Flushes

                                        0
                                     1113
                                      315
                                     1153
                                       53
                                      862
                                      730
                                      639
                                     1586
                                     1475
                                      291
                                       22
                                     1485
                                      932
                                      717
                                       35
Interval
 Urinal
 Flushes

     0
   727
   333
   810
    78
   657
   639
   540
  1008
   916
   262
    23
  1260
   561
   575
    76
Interval
  Waste
 (Gal.)

     0
    84

   174

    99
    77

   192

   209

   189

   178
     0
Note
Three women's and six men's restroom facilities connected to Aqua-Sans.

Example of Interval data:  Interval oil flow--6645 gal. total oil flow
between 0530 and 1650 hrs on 6/28.

-------
Table 5.  Oil Flow, Flush Count, and Waste Collection Data
July 31,  1972, Operating Period.
                   July 6, 1972,  Through
                      Interval Oil
                      Flow (Gal.)
Date
7/6

111

7/8

7/9

7/10

7/11


7/12


7/13

7/14


7/15

7/16

7/17

7/18


Time
0530
2130
0645
2130
1400
2130
1400
2130
1400
2130
0600
1400
2130
0600
1400
2130
1400
2130
0600
1400
2130
1400
2130
1400
2130
1400
2130
0600
1400
2130
Total :
0
4430
1006
4150
2307
1757
2874
1643
2572
1939
1021
2543
2372
1376
2046
1475
1691
1029
474
2346
1021
2714
1553
2232
1734
2424
1922
1059
2073
1382
Flushir
0
2575
60
2545
1065
975
1075
1015
1220
1055
50
1415
1150
205
1355
970
955
725
90
960
1135
1220
1010
1245
1350
1700
1240
165
1725
1070
  Interval
Water Closet
   Flushes

      0
    431
     10
    419
    175
    157
    180
    163
    199
    166
      8
    234
    187
     37
    221
    151
    147
    106
     14
    151
    210
    203
    159
    205
    218
    289
    198
     29
    294
    160
Interval
 Urinal
 Flushes

     0
  1032
    17
  1130
   477
   470
   439
   497
   562
   557
    18
   614
   532
    46
   631
   536
   553
   486
    48
   486
   212
   514
   533
   548
   654
   635
   627
    52
   634
   672
Interval
  Waste
 (Gal.)

     0
    84

   116

    77

    77

    95


   105


    84

    95


    66

    73

    84

    95


    84

-------
                                    Table 5.  (Cont.)
                            Interval Oil
                            Flow (Gal.)
Cn
Date
7/19

7/20

7/21


7/22

7/23

7/24

7/25

7/26

7/27

7/28

7/29

7/30

7/31

Time
1400
2130
1330
Out of
0600
1400
2130
1400
2130
1400
2130
1400
2130
1400
2130
1400
2130
1400
2130
1400
2130
1400
2130
1400
2130
0600
1700
Total :
2211
1166
1664
service

1842
1285
2061
2194
2782
2522
3096
1425
2628
1505
3205
1643
3578
1728
2288
1100
1693
1417
2291
1539
787
2944
Flushii
1655
1105
1290


1065
945
1535
1190
1070
1695
1605
975
1440
1165
1095
1165
1550
1165
1150
850
1075
675
1040
750
95
1675
  Interval
Water Closet
   Flushes

    282
    177
    212
    165
    149
    253
    194
    171
    288
    270
    155
    235
    182
    371
    175
    261
    190
    184
    133
    170
     98
    167
    113
     15
    295
Interval
 Urinal
 Flushes

   612
   548
   578
   593
   502
   663
   554
   541
   639
   642
   496
   668
   639
   599
   728
   610
   531
   569
   458
   562
   464
   506
   467
    55
   502
Interval
  Waste
 (Gal.)
                                                                                  105
                                                                                   31
    84

    95

    84

    84

    84

    95

    84

    73

    84

    73
      Note:  Six men's restroom facilities connected
             Example of Interval data:  Interval oil
             between 0530 and 2130 hrs on 7/6.
      to Aqua-Sans.
      flow--5530 gal.
    total oil flow

-------
Table 6. Hourly Oil Flush Flow Rates
Operating Period.
July 6, 1972, Through July 31, 1972,
Time
0600
0700
0800
0900
1000
1100
1200
1300
1400
1500
1600
1700
1800
1900
2000
2100
2200
6

_
0
100
270
240
253
279
184
236
261
154
166
39
110
104
56
7

_
.
.
_
_
_
_
_
_
111
174
123
36
109
63
154
8
.
-
_
-
_
_
-
-
-
160
169
148
134
84
99
68
118
9
_
-
49
45
172
106
236
161
228
193
171
164
153
106
150
74
76
10
_
-
57
46
160
165
285
181
258
248
320
129
81
97
61
78
80
11
„
-
41
103
233
278
183
258
255
169
178
208
117
192
145
181
98
Date
12
—
-
-
-
-
-
-
-
-
191
260
78
147
100
101
65
94
13
—
-
-
-
-
-
-
-
-
163
142
109
85
86
75
82
87
14
_
-
-
-
-
-
-
-
-
-
-
-
251
91
24
90
79
15
_
21
45
38
165
208
264
263
173
220
145
195
102
151
78
88
104
16
_
33
40
81
150
121
285
189
239
284
192
183
326
164
94
103
69
17
_
13
34
107
358
231
323
232
288
298
208
193
212
69
103
116
131
18
-
2
142
116
172
363
332
360
226
244
269
170
120
105
99
47
93

-------
                               Table 6. (Cont.)
Time
0600
0700
0800
0900
1000
1100
1200
1300
1400
1500
1600
1700
1800
1900
2000
2100
2200
19

15
46
97
180
365
-
-
-
269
270
219
236
58
76
-
-
20
.
3
19
56
150
385
151
360
-
-
-
-
-
-
-
-
-
21
_
12
14
96
213
138
279
173
49
216
271
139
121
79
83
61
114
22
.
15
28
77
242
265
241
257
291
202
257
210
137
168
111
85
84
23
.
-
-
35
95
116
224
200
319
314
317
291
211
254
208
81
132
24
_
42
58
137
176
198
338
221
294
237
166
166
131
56
70
122
141
Date
25
_
9
49
60
245
251
204
284
123
204
133
208
257
128
88
147
84
26
_
22
90
40
191
322
378
353
-
• -
224
176
102
135
211
184
150
27
_
26
46
91
223
325
276
140
293
216
273
217
136
82
76
144
139
28
_
20
28
18
180
130
238
230
268
-
-
59
56
59
19
78
70
29
_
67
60
67
86
80
260
173
179
88
156
138
52
105
26
83
252
30
_
38
-
-
Ill
93
253
202
197
149
190
148
97
66
92
92
194
31
_
17
17
129
205
248
137
29
110
-
-
-
-
-
-
-
-
Results in gallons

- indicates flow not recorded

Note:  Six men's restroom facilities connected to Aqua-Sans.

       Example of Interval data:  Hourly oil flow--100 gal. between 0800 and 0900
       on 7/6.

-------
The peak hourly flush flow of 385 gph represents a 6.4 gpm
average flush flow.  Based on a Peak to Average ratio of 3.44
as determined from the 5-minute data listed in Table 7, the
peak flow for the July 6 through July 31, 1972 period was 22
gpm.  Based on this peak flush flow, a 220 gal. waste sump
would provide a 10-minute theoretical detention time.  Fur-
ther discussion is presented on page 57.
Waste Sensors

The waste overfill sensor failed several times before the
capacitance was adjusted properly.  The waste sensor (lower
sensor) operated properly during the operating period.   How-
ever, failure of this waste sensor could have resulted in
the waste sump being emptied into the sewer while operating
automatically in the sewer mode.
Oil Reservoir Cleaning

Residue in the oil reservoir was originally removed by wash-
ing the surfaces with water and then pumping the accumulated
water into the waste sump via the recirculating pump.  This
produced high concentrations of suspended solids in the oil
because of turbulence near the waste/oil interface.  The pres-
sure differential across the primary filter increased rapidly
when the reservoir was cleaned in this manner.  A hose was
then connected to the suction side of the recirculating pump
and the residue was "vacuumed" from the reservoir into the
sump.  This method was time-consuming and could only be done
during no-use periods.  Only a small portion of the reservoir
could be cleaned before the oil overflowing the waste sump
became cloudy.  This cleaning method was continued to the end
of the demonstration period.  Proper design of the sump and
reservoir for solids carryover and eliminating areas for
solids and urine accumulation will eliminate the need for
reservoir cleaning.


System Vent

Positive venting was required to control odors in the reser-
voir.  The vacuum pump was originally vented with the reser-
voir, but separate, powered vents had to be installed to
eliminate odor problems around the Aqua-Sans unit.
Miscellaneous

The metering tank flow switch failed to shut the vacuum pump
off once.  The cause of failure was not determined.  The

                                  38

-------
         Table 7. Determination of Peak to Average Flush Flow Ratio
Date
Facilities

Flush
Flow
for
Five
Minute
Intervals

(gal./ 5 min. )



Average
Flow (gpra)
Peak Flow (gpm)
7/1/72
3 Women ' s
45
30
115
65
65
85
55
55
180




15.4
40.0
7/2/72
3 Women ' s
40
15
15
50
20
10
5
50





5.1
10.0
7/11/72
6 Men's
21
13
7
29
28
3
4
19
25
6
19
3

3.0
5.9
7/12/72
6 Men ' s
17
23
23
17
6
9
13
18
21
2
2
30

2.8
6.1
7/13/72
6 Men's
18
11
1
1
6
17
3
2
6
15
12
5

1.6
5.5
Ratio
(Peak/Average)
2.60
1.96
1.96
2.18
3.44
The peak flow is determined by the average number of flushes in a 5-minute period
with a fractional average of 1% meaning that at least 2 flushes occurred in one of
the one-minute intervals or the peak flow was 10 gpm.

-------
switch operated approximately 500 times with 80 percent of the
operation occurring after the one malfunction.

During the shutdown period after June 9, 1972, the accumula-
tor pressure switch failed to "pick up" and turn the primary
pump on when the pressure dropped to 30 psig.  The switch
started working after it was jarred several times.  An iden-
tical malfunction occurred one week later, with the switch
resuming proper operation after it was "jarred."  A new pres-
sure switch was installed prior to the June 28, 1972, restart.


OIL MAINTENANCE AND QUALITY

Oil maintenance consists of:  (1) removing the suspended
solids and water from the oil; (2) removing dissolved and very
fine suspended contaminants from the oil; (3) disinfecting the
oil; (4) eliminating odors from the oil; and (5) replacing oil
lost from the system.  The coalescer and the primary filter/
coalescer were installed to remove the suspended solids and
water from the oil.  The bypass filter system was installed
to remove the dissolved contaminants which caused color, odor,
and reduced the oil interfacial tension.  Biocides were added
to the oil as disinfectants.  Each of the individual oil
maintenance categories are discussed in the following subsec-
tions.
Suspended Solids and Water Removal

While most of the solid and liquid wastes were effectively
separated from the oil in the waste sump, colloidal and
finely divided suspended particles and water were carried
from the sump to the reservoir.  A large portion of these
solids and liquid eventually settled out in the oil reservoir
The solids collected on the flat or slightly sloped surfaces
in the reservoir, and the liquid eventually drained to the
low end of the reservoir to be pumped back to the sump.

The initial operating plan was to replace the three filter/
coalescer elements when the differential pressure reached
10 psid.  As shown in Table 8, the maximum primary filter/
coalescer element differential pressure was 4 psid.  The
filter was changed in July after more than four times as
much waste had been collected as in April.  The differential
pressure was 4 psid prior to both changeouts.  During filter
replacements it was observed that both the inlet and the out-
let sides of the elements contained waste particles.  Strong
odors were apparent during each replacement.   These observa-
tions indicate that the primary filter elements are more
                               40

-------
effective as an absorbing surface than as a filter and sug-
gest that the primary filter/coalescer entraps waste which
becomes the cause of odor.
Table 8. Primary Filter/Coalescer Element Replacement Record
  Date
 Filter
 Change

4/18/72
5/13/72
   Filter
Differential
  Pressure
   Cpsid)
7/12/72
  Total
  Waste
Collected
  (Gal.)

400 + (1)
               340
               1850 + (2)
        Comments

Strong waste odor and
waste coating inlet and
outlet sides of elements

Chlorox periodically
added to system between
5/1/72 and 5/10/72.
Elements cleaner and
less odor.

Strong waste odor and
waste coating
(1) No waste collection data for the 4/1-4/6 period.  Esti'
    mate 80 gal. collected.

(2) No waste collection data for the 6/5-6/9 period.  Esti-
    mate 500 gal. collected.
The primary filter/coalescer was effective in removing water
from the oil except during very high usage periods.  As will
be discussed in the following subsection, only three oil
samples collected during the demonstration had a water con-
tent above saturation.
Bypass Filter System

The initial bypass filter system consisted of an attapulgus
clay filter which was installed to remove color, dissolved

                          41

-------
contaminants, and finely divided suspended solids.  The
average bypass flow rate was maintained close to 1 gpm.
Operation with the one clay filter continued until the May
15, 1972, shutdown.  Table 9 shows the oil test results and
clay filter changes for February 6 through May 15, 1972.
The first two clay filter elements were changed before they
had been depleted.

The Givaudan G-4 was dissolved in acetone and the acetone
saturated the clay filter.  The large drop in IFT and color
rise between March 27 and April 3, 1972, is a result of the
March 29 addition of G-4.  Because of the inaccuracies
involved in the oil rise on filter paper method for deter-
mining IFT (explained in Section VII), the low IFT was not
detected and the clay filter was not changed until April 18,
1972.

The clay filter element was replaced April 18 and the IFT
rose to 28 dynes/cm and the color dropped from 50 to 10 units.
The IFT slowly dropped and the color increased in the follow-
ing operating period.  The single clay filter was capable of
removing oil contaminants from approximately 5500 gal. of
recirculated flush oil required for 1450 flushes.

During the shutdown period following May 15, 1972, additional
bypass filters, as explained in Section IV, were installed.
The method of IFT determination was also changed at that
time.  An additional sample valve was installed making it
possible to obtain oil samples from the primary filter  (bulk
oil) and the outlets of the clay and carbon filters.

Operation was resumed June 5 and was halted on June 9.  Table
10 shows the IFT and color results for the samples taken
during the five-day period.  The IFT of the bulk oil was
always lower than that from the bypass filter outlets, indi-
cating that the bypass filters were effective.  The oil color
increased from 10 to 20 units during the operating period.
During this period, approximately 20,000 gal. of oil were
required to transport the waste of 9,200 flushes.  The bulk
oil IFT was slightly lower than 30 dynes/cm when the system
was shut down June 9.

Operation was resumed June 28 after the macerator pump was
replaced and continued through July 31 (see Tables 11 and
12).  Table 11 shows that on June 29 the system received 2600
flushes.  This overload resulted in the IFT of the oil from
the clay filters dropping below the bulk oil IFT.  The car-
bon filters, however, remained effective.

The clay filters were replaced July 2 and the bulk oil IFT
dropped to 30 dynes/cm on July 5.  Three oil samples had


                               42

-------
Table 9. Oil Interfacial Tension and Color and Clay Filter
Changes.  February 6, 1972, Through May 14, 1972, Operating
Period.
                         Interval    Interfacial
         Interval          Waste       Tension        Color
Date      Flushes          (Gal.)      (dynes/cm)     (units)

 2/6     Start of demonstration period                  0
2/15        345          29.5             -             0
2/21        573          27.0            33.0           0
         Changed clay filter element
2/28        353          30.5            34.0           0
3/24       1710         130.5            31.3           0
         Changed clay filter element
3/27        407          31.5            28.0          10
3/29     Added G-4 Biocide
3/31        582          42.0 (est)       -            40
 4/3        643          47.0 (est)      17.8          40
 4/7        457          33.0 (est       20.5          40
4/12         -              -            20.0          40
4/14        880          74.5             -            40
4/17        565          38.0             -            50
4/18     Changed clay filter element and primary filter
         elements and cleaned reservoir
4/19         -              -            28.0          10
4/21        301          24.0 (est)      26.6          15
4/24        575          49.5             -            25
4/28        495          29.0             -            40
 5/1        676          59.0             -            45
 5/5        296          39.0             -            50
 5/7        624          42.0            15.8          50
5/12        601          49.0             -            55
         Changed clay filter element
5/13         -              -            25.5          50
5/14       1009          73.0             -            50
5/15     System operation temporarily halted


Note:  Three women's and six men's restroom facilities  con-
       nected to the Aqua-Sans.

- Indicates no data available.

Oil samples taken from outlet of clay filter (SV-2).

Interfacial tension results supplied by CCSD -  oil sample
and urea in equilibrium.

Example of Interval data:   Interval flushes--345 flushes
between 2/6 and 2/15.

                             43

-------
water contents above saturation during this period.  The
three women's water closets were switched to water prior to
the July 6 morning usage.

Table 12 lists the oil test results for the remainder of the
operating period with the six men's facilities in use July
1 through 31, 1972.  The bypass filters maintained the bulk
oil IFT above 30 dynes/cm during this operating period.  The
15,190 flushes (16,000 users) between the July 7 and July 17
bypass filter changes represented the maximum total usage for
the modified bypass filter system.  During this period the
oil had a yellowish color (30-45 units) and occasionally pro-
duced disagreeable odors in the restroom.
Table 10. Oil Interfacial Tension and Color.
Through June 9, 1972, Operating Period.
                                       June 5, 1972,
Date   Time
6/1
6/5

6/6

6/7
6/8

6/9
                  Interfacial Tension
       Interval        (dynes/cm)
        Flushes   SV-1   SV-2    SV-3
All filters replaced prior to start-up
0915
1400
0600
1530
1420
0500
1400
2000
   0
 493
 871
1073
1095
 622
 572
1591
System
38.9
37.5
34.3
29.8
36.5
34.0
29.5
restart
46.2
41.1
37.0
39.2
37.6
39.6
34.6

46.7
41.9
38.4
-
-
-
-
                                    Color
                                   (units)
                               SV-1 SV-2 SV-3
10
10
15
10
10
20
10
10
15
Note:  Three women's and six men's restroom facilities con-
       nected to the Aqua-Sans.

- No data available.

Interfacial tension determined for oil - water not at
equilibrium.

SV-1, SV-2, and SV-3 are sample values for bulk oil, clay
filter outlet, and carbon filter outlet, respectively.

Example of Interval data:  Interval flushes--493 flushes
between 0915 and 1400 on 6/5.
                                  44

-------
Table 11. Oil Interfacial Tension and Color
Replacement.  June 28, 1972, Through July 5
Period.
                              and Bypass  Filter
                               1972,  Operating
Date   Time


6/28

6/29

6/30

 7/1
 7/2


 7/3

 7/4

 7/5
           Interfacial Tension
Interval        (dynes/cm)
 Flushes   SV-1   SV-2    SV-3

0530
1650
0800
2030
0530
1745
1400
0615
0800
2130
1645
2130
0600
2130
1400
2130
Changed
0
1840
648
1963
131
1519
1369
1179
Changed
2594
2391
553
45
2745
1493
1292
clay filter elements
Operation restarted
38.0
36.9
37.5
35.6
44.0
37.9
40.0
39.2
41.9
33.3
33.7
' -
36.4
-
44.7
41.9
-
38.9
-
40.3
-
clay filter elements
41.5
34.0
42.0
42.7
33.6
30.6
30.0
-
35.7
'
43.1
-
32.2
-
-
-
•
-
-
.
-
     Color
    (units)
SV-1 SV-2 SV-3
                                  35
                                  45
                                  35
                                  30
                                  40
                                  50
                                  35
      30
      30
      30
      25

      45
                                  35   -
                                  40*  40*
                                  45
                                  40   40
                                  45   -
                                  35   40*
                                  45
30
25

25

45
Note:  Three women's and six men's restroom facilities con-
       nected to the Aqua-Sans.

- No data available.

* Samples were cloudy.

Interfacial tension determined for oil-water not at equilib-
rium.

SV-1, SV-2, and SV-3 are sample values, for bulk oil, clay
filter outlet, and carbon filter outlet, respectively.

Example of Interval data:  Interval flushes--1840 flushes
between 0530 and 1650 on 6/28.
                             45

-------
Table 12
Changes.
Period.
   Oil Interfacial Tension and Color and Bypass Filter
   July 6, 1972, Through July 31, 1972, Operating
                         Interfacial Tension
                                             Color
Date

 7/6

 7/7



 7/8

 7/9

7/10

7/11


7/12


7/13

7/14


7/15

7/16

7/17



7/18


7/19

7/20


7/21
Time

0530
2130
0645
0830
1400
2130
1400
2130
1400
2130
1400
2130
0600
1400
2130
0600
1400
2130
1400
2130
0600
1400
2130
1400
2130
1400
2130
1200
1300
1400
2130
0600
1400
2130
1400
2130
1000
1330
2200
1400
2130
Interval
Flushes

1574
27
Changed

1549

1279

1279

1484


1593


1622

1292


1131

1409

1625
924
Removed

825


1841

1619
Replaced
790
(dynes/cm)
SV-1
31
34
32
both
35
36
37
36
36
38
38
36
37
37
38
37
36
34
39
32
35
31
36
35
36
32
34
39
clay
33
41
43
31
33
33
33
one
33
.9
.2
.9
clay
.5
.9
.5
.2
.5
.4
.2
.5
.5
.8
.0
.8
.9
.9
.2
.6
.4
.0
.8
.3
.2
.2
.1
.2
SV-2
32
35

fi
40





41

40
39

39
41

36

39
35

29



39
filters
.2
.2
.1
.9
.6
.5
.0
clay
.1







.1
.3
-
Iters
.6
-
-
-
-
-
.6
-
.1
.6
-
.4
.5
-
.5
-
.4
.9
-
.5
-
-
-
.8
SV
32









40

40
37


33

36

42
34






-3
.8
-
-

-
-
-
-
-
-
.8
-
.0
.5
-
-
.3
-
.4
-
.3
.8
-
-
-
-
-
-
- Replaced
-
-
-
-
-
-
-
filter

-
35
44
42
31

35
33
and
33
.7
.0
.5
.3
-
.0
.5
(units)
SV-1 SV-2
40
45
40

35
40
40
35
35
35
35
40
35
40
40
40
35
40
30
30
30
40
35
35
35
40
40
45
carbon
40
35
30
35
40
35
40
40
40
-

35
-
-
-
_
-
30
-
30
35
-
35
35
-
30
-
30
35
-
40
-
-
-
40
fil
-
-
-
-
-
-
-
sv-
40
-
-

-
-
-
-
_
-
30
-
35
35
-
-
35
-
30
-
30
35
-
-
-
-
-
-
ters
40
30
25
35
-
35
40
both carbon filte
.8
40
-
35
                1409
35.6     -     33.2    40   -     40
35.3   39.5    41.0    35   30   30
35.9   39.4    41.4    35   30   35
                             46

-------
                 Table 12.  (Cont.)
Date
7/22
7/23

7/24

7/25

7/26


7/27

7/28

7/29

7/30

7/31

Time
1400
2130
1400
2130
1400
2130
1400
2130
1500
1500
2130
1400
2130
1400
2130
1400
2130
1500
2130
0600
1700
Interval
Flushes
1664
1639

1563

1724
Replaced
970
903

1592

1344

1294

1253

867
Interfacial Tension Color
(dynes/cm) (units)
SV-1 SV-2 SV-3 SV-1 SV-2 SV-3
36.2 39.8 - 35 30 -
35.3 - 40
33.6 - 40
34.
35.
35.
37.
39.
both
33.
36.
37.
36.
37.
40.
36.
38.
40.
41.
40.
38.
8
5
4
2
8
clay
0
8
9
1
4
6
5
6
0
0
6
1

34

35

_
.2
_
.8
-
and
35

39

40

36



43
41
.8
-
.8
_
.2
-
.4
_
-
-
.2
.0

35

37

both
35

40



38



41
40
—
.8
_
.2
_
carbon
.4
_•
.9
_
-
_
.8
_
-
_
.5
.6
40
40
35
40
35
_
40

35

_
35

35

filters
40
35
40
30
35
30
40
35
40
35
35
35
35

40

35
.
35

_
_
35
30
40

35

_
_
35

_
_
30
30
-No data available.

Interfacial tension determined for oil - water not at
equilibrium.

SV-1, SV-2, and SV-3 are sample values for bulk oil, clay
filter outlet, and carbon filter outlet, respectively.

Note:  Six men's restroom facilities connected to Aqua-Sans.

Example of Interval data:  Interval flushes--1574 flushes
between 0530 and 2130 on 7/6.
                             47

-------
Bacteria Control

Maintaining a zero bacteria population in the oil is desirable
for hygienic reasons and odor control.  Biobor JF was the pri-
mary method of bacterial control used during the demonstration
period.  Two attempts were made to get Givaudan G-4, a longer
lasting biocide, in solution with the oil.  The technical data
for both biocides are presented in Appendix D.

Initially, 135 ppm (chemical) of Biobor JF was added to the
oil weekly.  The amount was increased to 185 ppm on March 22,
1972, after two samples had low coliform bacteria counts.
Table 13 lists the results of all coliform bacteria tests and
the date biocide was added to the oil.

The first attempt on March 29 to get G-4 in solution with the
oil was apparently not successful, since a large amount of
the chemical was found in the reservoir.  In the month fol-
lowing the March 29 G-4 addition, there were three samples
which showed coliform bacteria; two of these had massive
populations.  There was no Biobor JF added during the period
from March 29 to April 27.

During the June 5 to June 9 operating period, massive coli-
form bacteria counts occurred on two successive days, with
250 ml of Biobor JF being added on the day prior to each
test.

One hundred ppm of G-4 (chemical dosage) was added to the oil
on June 22.  During the June 28 to July 5 operating period,
Biobor JF was added either daily or every other day.  Only
one sample showed coliform bacteria during this period.  The
system usage was higher than the usage between June 5 and
June 9, when bacteria were present in the oil, so apparently
the G-4 assisted the Biobor JF in killing bacteria in the
mineral oil.

Biobor JF was added to the oil in two- and three-day incre-
ments during the July 6 to July 31 operating period.  During
this period, three samples showed coliform bacteria.
Odor Control

The main problem, and the one not resolved, was odor.  The
odor problem affected both the operating area and the rest-
rooms.

As discussed in the previous section, there was usually no
bacteria population in the oil; however, the organic waste
material which collected in the oil reservoir and absorbed

                               48

-------
      Table 13. Biocide Addition Record and Coliform  Bacteria  Test  Results
Date
Interval
  Flush
   Oil
 (Gal.)
 Coliform
 Bacteria
(Colonies)*
1/31
2/8
2/15
2/17
2/21
2/22
2/28
3/3
3/10
3/17
3/22
3/24
3/27
3/29
3/31
4/3
4/7
4/14
4/17
4/19
4/21
4/28
5/5
5/12
5/15
6/1
6/5
6/6
-
-
660
150
1410
-
1140
315
1090
1385
-
2180
1190
Added G
1630
1885
1360
2440
1575
-
805
2840
3270
3755
System
-
System
4310
-
0
-
0
-
-
0
4
1
0
-
0
0
-4 Biocide
0
0
8
0
-
300
0
100
2
0
off line
. -
restart 0
0
 Biobor
   JF
Addition
 (ml) (2)

   180
   180
   180
                                  180
                                  180
                                  180
                                  250

                                  250

                                  (1)
                                  CD
                                  (1)
                                  (1)
                                  CD
                                  (1)
                                  (1)
                                  250

                                  250

                                  250

                                  250



Date
6/7
6/8
6/9
System
6/19
6/22

6/27
6/28
6/28
6/29
6/29 .
7/1
7/3
7/4
7/4
7/5
7/6

7/6
7/7
7/7
7/8
7/10
7/10
7/11
7/11
7/12
Interval
Flush
Oil
(Gal.)
6935
1910
3445
off line
-
Added G-4
(100 ppm)
-

Coliform
Bacteria
(Colonies)
100
100
6
Biobor
JF
Addition
* . (ml)
250
U)
(1)
(June 9 Flood)
-
Biocide to

0
250
system

250
System restart
5855
1710
6090
8675
19495
120
7930
4885
4020
Switched

2635
2545
1065
4285
1055
50
2565
205
0
6
0
-
-
-
0
0
0
women's side
0
0
3
-
-
100
0
0
0
-
250
-
250
250
250
-
250
250
to water
250
-
-
250
250
-
-
-
250

-------
                                    Table 13.  (Cont.)



Date
7/13
7/14
7/16
7/17
7/17
7/18
7/19
7/20
Interval
Flush
Oil
(Gal.)
3280
815
6920
1700
1240
165
5555
1290
 Coliform
 Bacteria
(Colonies)*

      0
      0
      0
      0
      0
      0
      0
     10
                                    Biobor
                                      JF
                                   Addition
                                    (ml)
                                      250

                                      250



                                      250



Date
7/21
7/22
7/23
7/25
7/26
7/29
7/30
7/31
Interval
Flush
Oil
(Gal.)
2010
1535
-
9040
2095
6955
2465
95
                                                                 Coliform
                                                                 Bacteria
                                                                (Colonies)*

                                                                      0
                                                                      0

                                                                      0
                                                                      0

                                                                      0
                                                                      0
 Biobor
   JF
Addition
  (ml)
   250

   250
   250
en
O
- Indicates no data available.

* 1 ml trypticase-soy-broth added to 10 ml oil and centrifuges for 10 min.  0.1 ml of
  extract streaked on agarplate,

(1) Ran out of Biobor JF.

(2) 180 ml (135 ppm)
    250 ml (185 ppm)

Example of Interval data:  Interval flush oil--660 gal. between 2/8 and 2/15.

-------
on the primary fliter/coalescer elements was not oxidized by
the biocide added to the oil.  The G-4 was soluble only in
oil and the Biobor JF soluble in oil and water.  The Sontex
60T mineral oil contained an oxidation inhibitor, Parabar
441, to prevent color changes due to oxidation of the oil.
The oxidation inhibitor tended to prevent oxidation of the
organic waste material and neither of the two biocides had
sufficient contact with the organic material to permit oxi-
dation.

Chrysler Corporation Space Division has worked extensively
on odor control since June, 1972.  A summary of the Chrysler
Corporation Space Division findings concerning odor control
is presented in Appendix A.

Table 14 shows the results of the public acceptance question-
naires explained in Section VII.  There were 72 question-
naires returned representing 643 urinal users and 30 ques-
tionnaires returned representing 230 water closet users.
Thirty percent of the urinal users and 18 percent of the
water closet users stated that the odor was objectionable.

The public acceptance of the oil color is also given in
Table 14.  Nine percent of the urinal users and 33 percent
of the water closet users indicated that the oil color was
objectionable.


Oil Loss

There were many forms of oil loss, but loss of oil with the
waste caused the greatest concern.  Oil losses were caused
primarily by turbulence in the waste sump during high use
periods combined with the short detention time (average of
less than one hour) between dumps.  Table 15 lists the oil
lost with the waste during the periods of time when it was
possible to determine all volumes of oil in the system and
waste in the sump.

During low-use periods, the rate of oil loss with the waste
was 3.8 gal./lOOO gal. of waste.  During the high-use period
starting June 28, the loss was 47 gal./lOOO gal. of waste.
                           51

-------
                 Table  14.  Results  of  Public  Acceptance Questionnaires
in
t-o
Date §
Time
Interval
7/27
1500-1800
7/28
1700-2100
7/30
1700-2100
Total
7/27
0700-1000
7/29
1400-2100
7/30
0700-1200
7/31
Total
(excluding
7/31)
Number Satisfactory wot &arisra<
Number Quest. Percent
Users Returned Return
252

190
201
643

66

99
65
Not
Recorded

230
31

25
16
72

11

13
6
31

30
12.3

13.1
8.0
11.2

16.7

13.1
9.2
_ - — _

13.0
Facility Color Odor
Urinals

Urinals
Urinals
Urinals
Water
Closets
Water
Closets
Water
Closets
Water
Closets

Water
Closets
28 18

23 20
10 11
61 49

9 10

5 9
5 5
22 26

41 50
Gen.
App.
26

23
11
60

10

8
6
24

48
Percent
Satisfactory
Urinals



Water Closets



Color
Odor
Color
Odor
91
70
67
82




Not




Color Odor
3

2
1
6

2

8
1
9

20
Percent
11

5
5
21

1

4
1
5

11

; LUI )
Gen,
App,
4

2
1
7

1


0
7

13

Satisfactory
9
30
33
18








    Note:  Men's restroom only.

-------
              Table 15. Oil Lost with Waste
              Oil Loss
                with       No. of                     (Gal./
            Waste Dumps     Waste      Oil Loss     1000 Gal
  Date          (Gal.)       Dumps    (Gal./Dump)      Waste)

4/21/72          0.8         18          0.04          3.8
   to
 5/5/72

6/28/72         13.0         23          0.56         47.0
   to
6/30/72

7/12/72          9.0         46          0.20         19.0
Several checks were made to determine the amount of oil being
lost with the waste by allowing the waste to sit in the
metering tank before macerating and pumping it to the sewer.
After a few minutes in the metering tank, oil would rise to
the surface of the waste.

The mode of operation was switched to "incinerator" so that
the overfill waste sensor would initiate a waste dump.  This
resulted in the waste level in the waste sump fluctuating
between 25 and 35 gal. at all times.  The amount of oil loss
per waste dump was reduced.

The rate of oil loss during the operating period with only
the men's restroom facilities connected to the Aqua-Sans
system was 19 gal./lOOO gal. of waste.  The reduction in oil
loss was a result of the increased detention time and the
increased volume of waste retained in the waste sump.


Useful Life of Mineral Oil Flush Fluid

No accurate prediction of oil life can be made based on data
collected during the demonstration period.  The useful life
of the mineral oil as a flush fluid appears, however, longer
than the five-month operation period conducted at Mount
Rushmore.  No reduction in serviceability was detected during
this period.  Proper filtering is essential, however, to
maintain the oil in a serviceable condition.
                          53

-------
Miscellaneous

Appendices B and D contain Chrysler Corporation Space Divi-
sion information on "Flush Fluid Specifications" and "Effects
of Flush Fluid on Humans," respectively.
RESTROOM FACILITIES

Several problems were encountered in the restroom facilities
which must be considered whenever an Aqua-Sans system is to
be used.
Flushing

The six water closets were rim flush-siphon jet water closets.
Fecal matter tended to settle rapidly out of the oil in the
water closet bowls.  Fecal matter would stick to portions of
the porcelain bowl.  Toilet paper would then stick to the
fecal material.  Paper continued to build up in the bowl until
a plug-up and runover occurred.  Increasing the flush volume
from four to five gal. per flush partially relieved the prob-
lem.  The inside surfaces of the water closets were also
sprayed with "FluoroGlide," a fluorocarbon (Teflon) based
solution.  The Teflon coating did help prevent the fecal mat-
ter from sticking.  Experience indicated that a Teflon coat-
ing would have to be applied monthly to the closet bowls to
prevent fecal matter and toilet paper accumulations.


Oil Spillage

A few instances of oil spillage occurred because of water
closet overflows.  Oil spillage occurred as a result of uri-
nal overflows on three successive evenings in May.  Operation
of the Aqua-Sans system was temporarily discontinued.  The
system was restarted June 5, 1972, with full-time restroom
attendants available in both the women's and men's restrooms
in case of an oil runover.

During the remainder of the operating period, a few instances
of water closet overflows occurred and many cases of urinal
overflows occurred. The urinal flush volume was adjusted to
0.4 gal. per flush prior to the June 5 restart.  The drainage
from two of the urinals got progressively slower, and urinal
overflowing problems occurred.  The urine being transported
with the oil was undiluted when it came in contact with the
pipes, and buildups in the urinal drain pipes occurred at a
much faster rate with the mineral oil flush media than with
water.
                               54

-------
Several attempts were made to clean the drain pipes with a
3N solution of acetic acid.  While drainage improvements
were noted, they were short-term.


Oil Splashing

Small oil droplets usually splashed onto the seat during a
water closet flush cycle.  The oil did not evaporate, and
the droplets accumulated and became unsightly.

Several attempts were made to adjust the flush cycle to
eliminate the splashing, but each flush cycle adequate to
remove waste from the water closet resulted in oil splash-
ing.  A different water closet was installed in place of
one of those in use.  The new water closet reduced the
splashing but did not eliminate it.

Spring-loaded seats were ordered, but these did not arrive
prior to the end of the project.  These would definitely
help with the oil splash problem and may eliminate any oil
splashing onto the seat.


Cleaning

Conventional cleaning agents normally used for water closet
and urinal cleaning are not to be used with the mineral oil
flush media.  Two different cleaning agents were provided by
Chrysler Corporation Space Division during the demonstration
period.

The first cleaning agent was difficult to completely remove
from the surfaces inside the water closet bowl and tended to
compound the waste sticking problem discussed under "Flush-
ing."  The second supply of cleaning agent differed only
slightly from the first but did not have the removal problem.
The difficulty in removal may have been due mainly to insuf-
ficient dilution with water prior to use.

The urinals were very difficult to keep clean, and some of
the not satisfactory urinal odors were undoubtedly a result
of this.

The supply of cleaning agent was used up in July and the
water closets and urinals were cleaned with brushes and water.
This method appeared to be adequate for the water closets
(which had a teflon coating) but not for the urinals.

Chrysler Corporation Space Division's recommended restroom
cleaning procedures are listed in Appendix E.


                             55

-------
DESIGN CRITERIA

Waste Loading

One objective of the demonstration project was to gather use-
ful data for establishing design criteria.  In addition to
the Visitor Center restrooms, there are three other restrooms
at Mount Rushmore.  The waste loadings were determined for
restroom users and not for visitors to the Monument.

The number of individual water closet flushes was automati-
cally counted and the number of urinal flushes determined by
the total oil flow to the urinals.  The relationship between
facility users and flushes was determined from the number of
users continuously recorded by an observer while another per-
son recorded the number of flushes at five-minute intervals.
Five observations were conducted for either 40 or 60 minute
periods.

Table 16 lists the results of the five observation periods.
Based on 365 restroom facility users, the average ratio of
flushes per user is 0.95.  The maximum deviations recorded
were 1 user per 3 flushes and 3 users per 0 flushes.  The
general trend is for the flush per user ratio to decrease
as the number of users increases.

The waste collection data are presented in Table 17.  Except
for three short periods, the amount of waste collected was
determined.  Excluding these periods, 4,056 gal. of waste
were collected.  Based on 67,438 flushes, the average ratio
of gal. waste per flush is 0.060.  Using the 0.95 flush per
visitor ratio, the average waste collection per user is
0.063 gal.  This number is biased by the minimum ratio of
0.059 gal. per user determined for the July 6 through July
31 operating period with only the men's restroom facilities
connected to the Aqua-Sans system.  Excluding this period,
the average ratio is 0.070 gal. waste per user and is the
recommended value for design purposes.  The maximum ratio
determined was 0.085 during a nine-day collection period.

Waste samples were collected and analyzed for suspended
(volatile and fixed) solids.  Table 18 shows that the sus-
pended solids in the separated (concentrated) human waste
are 92 percent volatile.  The total suspended solids concen-
tration for the three collected samples ranged from approxi-
mately 0.9 to 3.6 percent.

Based on the maximum suspended solids measured, the 4660 gal.
of human waste collected during ,the operation period con-
tained 1400 and 131 Ib of total and fixed suspended solids,
respectively.


                                  56

-------
          Table 16. Restroom Facility Flushes per User Determination,
Study
Period
Date (Min)
7/1/72 40
7/2/72 40
7/11/72 60
7/12/72 60
Restroom Facility
Facilities Users
women's 38
3 water closets
women's 84
3 water closets
men's 21
3 water closets
men's 130
Facility
Flushes
41
85
28
109
Ratio
(Flushes/1
1.08
1.01
1.33
0.84
7/13/72
 Total
60
 3 urinals
3 water closets

    men' s
 3 urinals §
3 water closets
90
                                              363
                                                             83
                                             346
                                                              0.92
                                                    0.95
                  Maximum Deviations
                               1 user, 0 flushes
                               3 users, 0 flushes
                               1 user, 3 flushes

-------
Table 17. Waste Collection and Water Closet and Urinal Flushes
Operating
Period
2/6/72 -
2/29/72
3/1/72 -
3/31/72
4/1/72 -
4/6/72
4/7/72 -
4/16/72
4/17/72
4/20/72
4/21/72 -
5/14/72
6/5/72 -
6/9/72
6/28/72 -
7/5/72
7/6/72 -
7/31/72
Totals
(excluding
estimated
(2))
(excluding
Water
Closet


1,







2,

3,

11,

10,


peri
waste

(2)
7/6/72-7/31/72
period)
(all
values
i -r^ ^» 1 * * *1 *> *1 i



tn
623

263

549

665

130

225

439

408

026


ods
col

and
Flushes
Urinal
711

1,383

551

780

171

1,951

2,885

8,465

27,938


of
lection

the


Total
1

2

1

1



4

6

19

37




67

,334

,646

,100

,445

301

,176

,324

,873

,964




,438

Waste
Collected
(Gal.)
91

200
o ~\
80C2)

112
fy\
24(2)

340
r 71
503UJ

1,202

2,111




4,056

Ratio n N
Gal. Gal.Llj
Flush
0.068

0.075

(2)

0.077

(2)

0.081

(2)

0.061

0.056




0.060

User
0.072

0.079

(2)

0.081

(2)

0.085

(2)

0.064

0.059




0.063

operating



TOO



A A QIC
29


7C
,474


1 A 1
1,945


A A£ 1
0.066



0.070



(1) Based on 0.95 flush per user.



(2) Waste volume estimated.
                           58

-------
Table 18
Waste.
Suspended Solids Concentration of Concentrated Human
          Suspended Solids (mg/1)
    Total         Fixed         Volatile
    8,790

   26,280 ...

   36,100
          720

        1,600

        2,800
       8,070

      24,680

      33,300
        Percent
      Volatile

         91.8

         93.9

         92.4
System Sizing

The primary factor involved in system sizing is having the
waste sump large enough to provide sufficient detention time
for the waste to separate from the mineral oil transport
media.  The size determined below is for a sump properly
designed to have a minimum turbulence caused by the waste -
oil inflow and to have no other inflow during use periods.
The 3.44 ratio of peak flow to average flow, determined
from peak hourly flush oil flows, is applied to the average
ratio of peak hourly flush oil flow  (Table 6) to average
hourly flush oil flow.  Table 19 lists these ratios for nine
days which had peak hourly flush oil flows exceeding 300
gph.  The average ratio is 2.40.

Multiplying the two ratios gives a ratio of peak flow  (deter
mined for 5-minute intervals) to average flow (determined
for daily operating periods) equal to 8.3.


Table 19. Determination of Peak Hourly Flow to Average Flow
Ratio.
    Date

    7/10
    7/16
    7/17
    7/18
    7/19
    7/23
    7/24
    7/26
    7/27
     Flush Oil Flow (gph)
      Peak        Average
     Hourly       Hourly
      320
      326
      358
      363
      665
      319
      338
      378
      325
                   Average
   120
   136
   154
   156
   145
   145
   136
   173
   143
ratio
     Ratio
(Peak/Average)

      2.67
      2.40
      2.37
      2.39
      2.52
      2.20
      2.48
      2.18
      2.27
      2.40
                             59

-------
The sizing of the waste sump for a certain number of daily
users  is dependent upon the number of hours a facility is
open,  the ratio of women to men users, the volume of oil
.required per flush, and the ratio of water closets to uri-
nals in the men's restroom.  The data were collected when
the visitor center restrooms were open 19 hours a day.  The
average ratio of urinal flushes to men's water closet flushes
is difficult to determine, since there were six water closets
in the men's restroom and only three of these were connected
to the Aqua-Sans system.  Using an equal ratio of water
.closets to urinals, a 2.86 ratio of urinal users to water
closet users was determined for Mount Rushmore.  This ratio
would  probably be higher if there had been more urinals
available for use.

Table  20 indicates that the waste sump size is highly depen-
dent on the ratio of water closet flushes to urinal flushes
and the volume of oil required per flush.

The waste collection, bypass filter element replacement, and
biocide addition requirements per 1,000 users are 70 gal.
waste, 16-day intervals, and 185 ppm of Biobor JF every three
days,  respectively.
WATER CONSERVATION

The use of the Aqua-Sans system  for  transporting human wastes
at Mount Rushmore resulted  in a  total  local water  saving of
240,000 gal., with  175,000  gal.  being  conserved between June
28 and July 30.  These figures were  determined by  multiplying
the number of water closet  flushes by  5 gal. per flush and
the number of urinal flushes by  2 gal. per flush.  Both flush
volumes are conservative figures for restroom facilities uti-
lizing flushometer  valves.

In addition to the  water conservation  achieved, the hydraulic
load to the Mount Rushmore  septic tank-sand filter sewage
treatment facility  resulting from the  79,000 Aqua-Sans users
was reduced 98 percent.
SUMMARY OF EVALUATION RESULTS

There was 4660 gal. of concentrated waste collected from
79,000 Aqua-Sans users during the five-month demonstration
period.  The cumulative processed and recirculated flush oil
was 173,000 gal.  This oil was required for 30,328 water
closet and 44,825 urinal flushes.
                                  60

-------
Table 20.  Sump Size, Waste Collection, and Maintenance as a
Function of Users
Daily Usage

Daily Oil
Flow (Gal.)
Waste Sump 7
Size (Gal.)
Daily Waste
(Gal.)

Bypass
Flush
19 hr.
day
0
2,880
0
-
500 Men
500 Women
2,880
2,140
230
1*000
Men^
2,880
1,530
113
1,000
Women
2,880
4,750
350
12 hr.
                                      364
70
          178
                                   70
554
 70
Biobor JF added every 3 days--250 ml  (185 ppm)

Bypass filter elements  (2 clay, 2 carbon) replaced every 16
days.
 0.95 flush per user, 5 gal. water closet flush, and 0.4 gal.
urinal flush.

 Providing 10 minutes theoretical detention time.

 Assuming 8.3 ratio still applies.

 2.86 urinal flush per water closet flush.
                             61

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Turbulence in the waste sump resulted in excessive waste
carryover from the waste sump into the oil reservoir.  Inlet
conditions were the primary cause of the turbulence during
"low use" periods.  During "high use" periods, the turbulence
was increased because of the high flush oil flow rate and
corresponding short detention time in the waste sump.

Bacteria control in the oil is possible through the proper
addition of biocides.  However, neither of the two biocides
used controlled bacterial growth in the organic material
which accumulated in the oil reservoir and on the filter ele-
ments.

Odor in the oil and around the Aqua-Sans system resulted from
the bacterial growth in the organic accumulations.  A forced
draft on the reservoir vent will reduce the odors around the
system.  An oxidizer capable of oxidizing any organic mate-
rial that collects outside the waste sump is necessary.

The bypass filter system with 2 clay filters and 2 carbon
filters maintained the oil IFT above 30 dynes/cm for 16,000
users.  The bypass filters also maintained the oil color
below an acceptable 55 units throughout the demonstration.

Most public objections to the oil flush were due to color and
odor.  Thirty percent of the urinal users objected to the
odor and 33 percent of the water closet users objected to the
oil color.

Most of the separated waste was pumped to the Mount Rushmore
sewage treatment facility.  A commercial macerator with a 4
in. inlet adequately ground and pumped the waste.

The amount of oil loss with the waste was a function of the
facility usage rate and the operating level of waste in the
waste sump.

There were 0.95 flushes per facility user.  The average user
waste loading ranged from 0.059 to 0.085 gal. per user with
0.07 gal. per user recommended for design purposes.

The ratio of peak flow (gpm averaged over 5 minutes)  to
average flow (gpm averaged over 19 hrs) is 8.3.

Water conservation is achieved by using a recoverable, non-
aqueous flush media.  A total of 240,000 gal. of water was
conserved during the demonstration.

Problems were encountered in the restrooms as a result of
using the mineral flush media.  These problems were 1) waste
sticking, 2) oil overflows, and 3) oil splashing onto toilet
seats.

                                  62

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                      SECTION IX

                   ACKNOWLEDGEMENTS
The support and cooperation of the National Park Service,
Mount Rushmore National Memorial, under Park Superintendent
Wallace 0. McCaw, are gratefully acknowledged.

The support of the project by the Water Quality Office,
Environmental Protection Agency, and the assistance provided
by Mr. William Librizzi and Mr. Leo T. McCarthy, Jr., the
project officers, have been very much appreciated.

-------
                       SECTION X

                      REFERENCES
1.   "Standard Methods for the Examination of Water and
    Wastewater," 13th Edition, American Public Health
    Association, New York (1971).

2.   "1972 Annual Book of ASTM Standards," Part 29, American
    Society for Testing and Materials, Philadelphia,  Pa.
    (1972).
                          65

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                      SECTION XI

                       GLOSSARY


The following abbreviations and terms are used in this report.

cm   = centimeter(s)

 F   = degrees Fahrenheit

gph  = gallons per hour

gpm  = gallons per minute

gal. = gallon(s)

hp   = horsepower

IFT  = interfacial tension

in.  = inch(es)

ppm  = parts per million

psig = pounds per square inches gage-pressure reading refer-
       enced to atmospheric pressure

psid = pounds per square inches differential-pressure differ-
       ence between two locations


Accumulator - The system pressure tank.

Biocide - An agent which kills bacteria.

Coalescer - A device used for removing water from the mineral
     oil.

Interfacial Tension - A measurement of the force per unit
     length existing at the interface of two dissimilar
     fluids.

Macerator - A grinder-pump unit used for grinding and pumping
     the concentrated waste.

Waste Sump - The waste separation and waste storage tank
     located inside the oil storage reservoir.
                          67

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                    APPENDIX A

        CHRYSLER CORPORATION SPACE DIVISION
TECHNICAL EVALUATION OF AQUA-SANS TREATMENT SYSTEM
                           69

-------
 TECHNICAL REPORT                                                TR-RE-73-262
                             SEWAGE TREATMENT SYSTEM




                        DEMONSTRATION PROJECT FINAL REPORT



                                      FOR




                       BLACK HILLS CONSERVANCY SUB-DISTRICT
                                CONTRACT BH 61771
                                   JANUARY 1973
              Prepared  by:_
                            R. W.  Loomis,  Project Manager
             Approved by:_
                            V,  J.nVehko,  Director  of Engineering
Chrysler Corporation Space Division, P. 0. Box 29200,  New Orleans,  Louisiana   70189

-------
1.0           INTRODUCTION

     This final report documents the design, fabrication, installation and

operational test of a Chrysler Aqua-Sans sewage treatment system, which was

installed at the Mount Rushmore National Memorial Visitors' Center (figures 1

and 2).  The report includes test objectives and results, and conclusions

and recommendations based on Chrysler's review and analysis of test data.


     The Chrysler Aqua-Sans system uses a non-aqueous, recirculated flush

medium to transport human waste from the toilet facility to a separation

tank.  After separation, the waste can be incinerated, or disposed of with

a septic tank or aerobic system.


     Chrysler's contract with the Black Hills Conservancy Sub-District was
                                                  x
partially funded by a Class II demonstration grant from the EPA.  The pro-

ject objectives of that grant proposed to demonstrate the feasibility of

using a non-aqueous system for the collection, transport and disposal of

human waste, to demonstrate that water conservation could be achieved by

use of such a system and that the recycled flush fluid was acceptable for

the intended purpose.  In addition, operational maintenance techniques

were to be developed and demonstrated so that the concept could be sub-

sequently applied in remote areas where more conventional sewage treatment

methods were not: applicable.


     The major project objectives were achieved within the 18-month pro-

gram schedule.  The Mount Rushmore  unit was  the  first field installation of

Chrysler's sewage treatment concept, and there were system deficiencies

noted during the test program.  These problems were either resolved during

the program by system modification or have been resolved during concurrent

and subsequent development under other Aqua-Sans contracts and Chrysler

research and development.


                                   A-l

-------
Figure 1.  Mount Rushmore Visitors'  Center
Figure 2.  Restroom Building, Mount Rushmore
           Visitors' Center
                    A-2

-------
      Significant data were collected during the test program relating to

 high-use public restroom facilities
 2.0

 2.1
             DESIGN AND DEVELOPMENT
             CRITERIA

     System design criteria were based on rough estimates of facility usage

at Mount Rushmore as  expressed  in  Chrysler's  proposal MI-212A, dated May 20,

1971.  These criteria, and the actual design parameters of the delivered

system are shown in Table 1.


      	Table 1 - Design vs Delivered System Criteria
     Commode Uses/day

     Urinal Uses/day

     Flush Fluid Flow/day
     (capacity)

     Primary Pump  (capacity)

     Accumulator  (capacity)

     Waste (capacity)

     Main Tank  (capacity)
                                    MI-212A
                                    Criteria
                                     400

                                     600

                                  4000 gal


                                20 gpm at 50 psi

                                   100 gal

                                   120 gal

                                   300 gal
                                                        Delivered
                                                          System
     400

     600

  4000 gal


50 gpm at 50 psi

    60 gal

   120 gal

   360 gal
     A major constraint in the design of the unit was the requirement that

the system be installed in the Mount Rushmore Visitor's Center basement

through a 33-inch-wide door.  In order to meet this constraint, the tank,

tank stand, major functional components, and the incinerator were all

designed so that the system could be assembled on site*
                                    A-3

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2.2          SEPARATION SYSTEM




     A schematic drawing of the separation system is shown in figure 3.




Photographs of major elements are shown in figures 8, 9 and 10.  The




design of the major subsystems is discussed in the following paragraphs.






2.2.1        Flush Fluid Supply




     A 360-gallon separation tank (figure 4) was designed to store flush




fluid and provide a sump for temporary storage of separated waste.  This




stainless steel tank contains a barrel with a 100-galIon capacity which




serves as a first-stage separation container.  Flush fluid and waste from




the soil drain are introduced at the top of this barrel and separated flush




oil passes through a screen, over the circular weir and through a gross




coalescer.  Water which settles out from the coalescer is periodically




pumped back into the first stage barrel by a recirculating pump (figure 5).




The tank is fitted with a 3-section lid; the center section contains a




transparent window and a light for observation.  The tank is vented and




contains a flush fluid sight glass and overfill float switch,  (figure 1).






     A centrifugal pump is used to pressurize an accumulator and supply




the facilities with flush fluid.  The pump is rated at 50 gpm  at 50 psig




outlet pressure.  The accumulator contains a usable volume of  16 to 23




gallons, depending on line pressure and accumulator precharge.  The air




side of the accumulator is charged by the vacuum pump used to  transfer




waste.  The flush fluid pump is controlled by a pressure switch on the




air side of the accumulator.  A 4-element filter/coalescer is  installed




downstream of the pump; a bypass valve and relief valve are also in-




cluded.
                                   A-4

-------
        Figure 3. Separation System Mechanical  Schematic - legend
Number     Component Name

  1.    Vacuum Pump Inlet Valve
  2.    Metering Tank Vacuum Valve
  3.    Vacuum Pump Vent Valve
  4.    Macerator Pump Drain Valve
  5.    Sediment Drain Valve and
       Flush Fluid Fill Valve
  6.    Sediment Pump Inlet Valve
  7.    Sump Drain Valve
  8.    Waste Sensor Valve
  9.    Waste Overfill Sensor Valve
 10.    System Drain Valve
 11.    Inlet Screen Water Isolation
       Valve
 12.    Metering Tank Water Isolation
       Valve
 13.    Filter Drain Valve
 14.    Clay Filter Isolation Valve
 15.    Accumulator Charge Valve
 16.    Filter Drain Charge Valve
 17 .    Primary Filter  Isolation
       Valve
 18.    System Bypass Valve
 19.    System Shutoff  Valve
 20.    Primary System  Suction  Valve
 21.     System Relief Valve
 22.     Sensor Flush Valve
 23.     Incinerator Transfer Valve
 24.    Vacuum Breaker  Check Valve
 25.     Incinerator Transfer Control
       Valve
 26.     Water Flush Solenoid Valve
 27.     Vacuum Breaker  Solenoid
        Valve
 28.     Water Flush Check Valve
 29.     Sediment Pump Check Valve
 30.     Primary System Check Valve
 31.     Metering Tank Check Valve
 32.     System Pressure Gage
 33.    Primary System Pressure Switch
 34.    Accumulator
 35.    Clay Filter Differential
        Pressure Gage
  36     Clay Filter
  37.    Primary Filter Differential
        Pressure Gage
  38.    Primary Filter/Coalescer
  39.    Primary System Flowmeter
 40.    Primary Pump
  41.    Sensor Flush Check Valve
  42.    Recirculating and Sediment
        Pump
Number        Component Name

 43.       Macerator Pump
 44.       Vacuum Pump
 45.       Metering Tank Vent Float
           Valve
 46        Metering Tank Fill Float
 47.       Reservoir Overfill Float
           Switch
 48.       Waste Overfill Sensor
           (Approximately 32 gallons)
 49.       Waste Sensor
           (Approximately 12 gallons)
 50.       Filter Bleed Valve
 51.       Sample Valve
 52.       Pump Inlet Screen
 53.       Gross Coalescer
 54.       Strainer
 55.       Clay Filter Calibration
           and Sample Valve
 56.       Bypass Flowmeter
                                     A-5

-------
WATER
SUPPLY
                                                                                                             SYSTEM
                          SEWER
                             Figure 3.  Separation System Mechanical Schematic

-------
TO METERING
   TANK
                         SEPARATION
                         TANK

 1.  VACUUM PUMP INLET VALVE
 2.  METERING TANK VACUUM VALVE
 3.  VACUUM PUMP VENT VALVE
10.  SYSTEM DRAIN VALVE
13.  FILTER DRAIN VALVE
15.  ACCUMULATOR CHARGE VALVE
16.  FILTER DRAIN CHARGE VALVE
17.  PRIMARY FILTER ISOLATION VALVE
18.  SYSTEM BYPASS VALVE
19.  SYSTEM SHUTOFF VALVE
20.  PRIMARY SYSTEM SUCTION VALVE
21.  SYSTEM RELIEF VALVE
30.  PRIMARY SYSTEM CHECK VALVE
32.
33.
34.
37.
38.
39.
40.
44.
50.
51.
52.
53.
 SYSTEM PRESSURE GAGE
 PRIMARY SYSTEM PRESSURE SWITCH
 ACCUMULATOR
 PRIMARY FILTER DIFFERENTIAL PRESSURE GAGE
 PRIMARY FILTER/COALESCER
 PRIMARY SYSTEM FLOWMETER
 PRIMARY PUMP
'VACUUM PUMP
 FILTER BLEED VALVE
 SAMPLE VALVE
 PUMP INLET SCREEN
 GROSS COALESCER
                                                                                                                 SEWER
                                                                                           TO SENSOR FLUSH
                                                                                                         DRAIN
                               Figure 4.  Flush Fluid Supply Schematic

-------
                                          WASTE INLET
I
                 SEPARATION
                 TANK
FILL AND DRAIN
                                                 FROM FILTER DRAIN
                                                                                    FROM
                                                                                    ACCUMULATOR
            5. SEDIMENT DRAIN VALVE AND
               FLUSH FLUID FILL VALVE
            6. SEDIMENT PUMP IN LET VALVE
           14. CLAY FILTER ISOLATION VALVE
           22. SENSOR FLUSH VALVE
           29. SEDIMENT PUMP CHECK VALVE
           35. CLAY FILTER DIFFERENTIAL
               PRESSURE GAGE
           36. CLAY FILTER
                                                                             FROM ACCUMULATOR
                                                                                     22
                                  41. SENSOR  FLUSH CHECK VALVE
                                  42. RECIRCULATING AND SEDIMENT
                                      DRAIN PUMP
                                  48. WASTE OVERFILL SENSOR
                                  49. WASTE SENSOR
                                  53. GROSS COALESCER
                                  55. CLAY FILTER CALIBRATION AND
                                      SAMPLE VALVE
                                  56. BYPASS FLOWMETER
                                       Figure 5. Fluid Maintenance Schematic

-------
2.2.2        Fluid Maintenance



     In addition to the in-line filter mentioned in the previous para-



graph, an Atapulgus clay filter is used in a  1  to 2-gpm bypass system



to remove color and dissolved contaminants,  (figure 5)   During the



test period, an additional clay filter and a  2-element activated carbon



column were added to this bypass  loop for more  effective odor control.



A screen in the barrel and the gross coalescer  are designed  to remove



large particles and coalese water carryover  from the barrel.  This water



is periodically pumped back into  the sump with  a small pump.  Midway in the



demonstration program the coalescer was removed from the tank to reduce



solids carryover into the main tank, and the  screen in the barrel replaced



with a coalescer.  Bacteria control is achieved by periodic applications



of biocide, which is partially soluable in both oil and water.
                                                s




2.2.3        Waste Transfer



     Waste is transferred (figure 6) from the sump to a metering tank by



evacuating the metering tank with a vacuum pump.  This transfer cycle is



initiated by a capacitance probe  which signals  a transfer cycle when



approximately 12 gallons of waste have accumulated in the sump.  Waste



is transferred until actuation of a float switch in the metering tank



stops the pump and vents the tank.  From the  metering tank, waste flows



by gravity to the incinerator to  be burned or to the macerator for  trans-



fer to the sewer system.




2.2.4        Water System


     The water system  (figure 7)  provides water pressure to  actuate the



incinerator transfer valve and is routed to  two sprays which rinse  the
                                   A-9

-------
WATER SUPPLY
                VENT
                                    SANITARY DRAIN
                          SEPARATION
                          TAN K
                                   ,/V^>
TO INCINERATOR
                       DRAIN
                                            6-
                                                        FILL
                                                        ANJD
                                                        DRAIN
 7
23.

-
31.
43.
44.
45.
46.
48.
49.
VACUUM PUMP INLET VALVE
METERING TANK VACUUM VALVE
MACERATOR PUMP DRAIN VALVE
SUMP DRAIN VALVE
INCINERATOR TRANSFER VALVE
INCINERATOR TRANSFER CONTROL VALVE
VACUUM BREAKER SOLENOID VALVE
CHECK VALVE
MACERATOR PUMP
VACUUM PUMP
METERING TANK STOP VALVE
METERING TANK FLOAT SWITCH
WASTE OVERFILL SENSOR (APPROX. 32 GAL.)
WASTE SENSOR (APPROX. 12 GAL.)
            TO SEWER
                        Figure 6.  Waste Transfer Schematic

-------
WATER
SUPPLY
         25
                12
              46
11. INLET SCREEN WATER ISOLATION VALVE
12. METERING TANK WATER ISOLATION VALVE
25. INCINERATOR TRANSFER CONTROL VALVE
26. WATER FLUSH SOLENOID VALVE
28. WATER FLUSH CHECK VALVE
47. RESERVOIR OVERFILL FLOAT SWITCH
54. STRAINER
   INCINERATOR VALVE
                                                                      SEPARATION
                                                                      TANK
                                   TANK
                                Figure 7.  Water System Schematic

-------
VACUUM-LI FT PUMP
             Figure 8.  Separation System

-------
                                                WASTE
                                                TRANSFER
                                                VALVE
                                            VACUUM-LIFT
                                            PUMP
Figure 9.  Separation System

-------
                        INSTALLATION OF MAIN PUMP AND WASTE SUMP
                                 INCINERATOR CONTROL PANEL
I—1
4>
                 METERING TANK, WASTE VALVE,
                 AND ASSOCIATED PLUMBING
CLAY FILTER, FILTER SYSTEM, ACCUMU-
LATOR, AND ASSOCIATED PLUMBING
SEPARATION AND FLUSH FLUID
CONTROL PANEL
                                                    Figure  10.  Mount Rushmore Unit

-------
metering tank following a waste transfer cycle and periodically rinse




down the waste inlet screen.






2.3          INCINERATOR




     A 2-stage, oil burning incinerator (figure 11) fabricated of type




309 stainless steel, was designed for the system   The first stage con-




tains a crucible into which approximately 10 gallons of waste can be




transferred.  Exhaust gases are passed into a second stage where they




are maintained at 1100 to 1300°F for sufficient time to ensure complete




oxidation of exhaust products.  Both stages are insulated with ceramic




fibre insulation and are air cooled.








2.4          CONTROLS




     Control panels  (figures 10, 12 and 13) are installed on both the




separation  system and incinerator.  Test and automatic operation modes




are provided for all functional components with switches.  Status lights




indicate system condition, and audible and visual  alarms are provided




for critical operations.






2.5          INSTRUMENTATION




     Flowmeters are  provided to indicate  total primary pump output




(figure 4), and to measure bypass  flow rate  (figure  5).  Counters are




included to monitor  incinerator and macerator cycles, and  three  tempera-




ture indications are displayed on  the incinerator  control  panel  (figures




12, 13) .  The  Black  Hills Conservancy Sub-District provided flush counters




for each commode  (figure  14) and  a flowmeter  to monitor  urinal flush




volumes  (figure 15).
                                   A-15

-------
         10
t
  \t.
              t
ru_
\J>
              Fl
                                               TO CHIMNEY
JL*_
I
    1. MOTORIZED DAMPER
    2. POT BURNER-BLOWER ASSEMBLY
    3. STACK BURNER-BLOWER ASSEMBLY
    4. FUEL SOLENOID VALVES (4)
    5. FUEL PRESSURE GAGE
    6. WASTE BOILER
    7. POT TEMPERATURE SENSOR
    8. STACK QUENCH AIR BLOWER
    9. SECOND STAGE TEMPERATURE SENSOR
      (DAMPER CONTROL)
   10. STACK TEMPERATURE SENSOR
   11. WASTE INLET
       M - MOTOR   P - FUEL PUMP
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                      INCINERATOR
                                           FUEL RETURN

            Figure 11.  Incinerator System Mechanical Schematic
                          A-16

-------
                                               INCINERATOR CYCLE COUNTER    MACERATOR CYCLE COUNTER
                                                                          J
                   24 VAC
        INCINERATOR READY

           READY FOR DUMP
               TIMER NO. 1
    TRANSFER AND
    SENSOR FLUSH COMMAND
WATER FLUSH AND
RECIRCULATE PUMP COMMAND
        INCINERATOR START
               TIMER NO. 2
           SELECTOR SWITCH-
                 CB NO. 1
                 CB NO. 2

                 CB NO. 3
TEST SWITCHES
  o   o
WASTE OVERFILL

TANK OVERFILL

LONG DUMP

ALARM RESET SWITCH


•ALARM OFF LIGHT
                                        SENSOR FLUSH VALVE
                                                                                \      WATER FLUSH VALVE
                                 TIMER NO. 1    TIMER NO. 2        \       \     \    MACERATOR PUMP
                                               RECIRCULATING PUMP       \     VACUUM PUMP
                                                            TRANSFER VALVE
                                     Figure 12.  Separation System Control Panel

-------
                                     POT BURNER CONTROLLER

00
         SHORT BURN

         LONG BURN
         POT BURNER
       STACK BURNER'
     STACK OVERTEMP
      POWER FAILURE
  ALARM RESET SWITCH

    ALARM OFF LIGHT

CIRCUIT BREAKER NO. 2


CIRCUIT BREAKER NO.  1
                                                         I
                                                                        STACK OVERTEMPERATURE CONTROLLER
                                                                               DAMPER CONTROLLER
TEST SWITCHES
                                                   OOO O  GO
                           EMERGENCY-OFF SWITC
                                  INHIBIT-ARM SWITCH
                                   MANUAL START SWITCH
                                                          FUEL VALVE NO. 2
                                                       FUEL VALVE NO.  1
                                                     POT BURNER SWITCH
                                                                                             STATUS
                                                                                             o—
                                                                                             o-
                                                                                             o-
                                                                                             o
                                       -24 VAC
                                       •INCINERATOR READY
                                       -INCINERATOR START
                                       • POT BURNER ON
                                        STACK BURNER ON
                                                                                                       'UPPER BLOWER SWITCH
                                                                                                       'BURNER BLOWER SWITCH
                                                                                                  V
                                     FUEL VALVE NO. 2
                                   FUEL VALVE NO. 1
                                 STACK BURNER SWITCH
                                                Figure 13.  Incineration System Control Panel

-------
                                   ..   .4-.
Figure 14.  Commode Flush Counters
   Figure 15.  Urinal Flowmeter
              A-19

-------
3.0          FABRICATION AND CHECKOUT




3.1          SEPARATION SYSTEM




     The separation system tank was fabricated by Chrysler and the system




assembled at New Orleans.  Due to unanticipated delays in procurement of




some key components, the separation system was completed approximately 4




weeks behind the original schedule.  Checkout was accomplished early in




December 1971, with the performance of leakage, functional and integrated




subsystem tests.  During these tests, six pipe fitting leaks were re-




paired, transfer volumes and level sensors were calibrated and control




system function was verified.  After ten successful transfer cycles,




checkout was considered complete.  Following checkout, the system was




dissassembled, packaged, and shipped.  The unit arrived at Mt. Rushmore




January 7, 1972.







3.2          INCINERATOR




     Early in the program, a decision was made to subcontract the incinerator




fabrication to an outside vendor.  The unit was not delivered to Chrysler




until December, and some rework and a considerable amount of tuning/adjust-




ment of air flow control and burner nozzles was required before successful




waste burns were accomplished.  The incinerator was shipped assembled, and




arrived at Mount Rushmore February 2,  1972






4.0          INSTALLATION AND SYSTEM START-UP




4.1          SEPARATION SYSTEM




     Installation and checkout of  the separation system  (figure 16) was




successfully accomplished in 1 week.  Start-up procedures in the Operation




and Maintenance manual were verified and some changes recommended.  Facility




switchover from water flush  to oil flush and return was verified, and




sanitary napkins were successfully processed through  the macerator   The
                                  A-20

-------
Figure 16.  Separation System after Installation
                    A-21

-------
system was connected to the restroom facilities for a shakedown during




the week of January 15, prior to receipt of the incinerator   While




awaiting arrival and installation of the incinerator, collected waste




was macerated and pumped into the Mount Rushmore septic tank.






4.2          INCINERATOR




     The incinerator (figure 17) arrived at Mount  Rushmore February 2,




was then uncrated, dissassembled, moved to the basement of the Visitors'




Center and reassembled.  Initial tests were begun February 4.  Problems




with incinerator draft were immediately evident, due to altitude (1 mile)




and problems of sharing the Visitors' Center chimney.  These problems




are discussed in more detail in section 5.2.  During February, March




and April, the draft problem was investigated and a number of incinerator




modifications performed to induce an adequate draft condition.  A proper




draft condition is a requirement for this incinerator design since it is




a double-wall, air cooled unit.  Without proper draft conditions, the re-




quired air/fuel ratio could not be maintained, and cooling of the double-




wall chamber was marginal.  The draft problem was never completely re-




solved, and when results with another similarly designed unit indicated




that the insulation and the 309 CRES material used in the design had a




limited life, the decision was made to macerate and pump all waste to




the Mount Rushmore  septic system.






5.0          DEMONSTRATION TEST PROGRAM




5.1          TEST OBJECTIVES




     The following  test objectives were delineated in the Operational




Evaluation Test Plan, TP-RE-71-233  (reference 3) covering  the actual




operational evaluation of  the Aqua-Sans system at  Mount Rushmore:
                                  A- 22

-------
Figure 17.  Incineration System after Installation
                     A-23

-------
a.  The system can be started up at the site with all




    components operating satisfactorily.




b.  The system can be used in conjunction with a conventional




    sewer system, with the capability of changing back and




    forth from one system to another.




c.  The system can perform its functional task of disposing




    of human waste at the site.




    1.  The system can receive sewage at whatever rate




        delivered to it at peak as well as average and




        below average periods, and under the extremes




        of temperature anticipated.




    2.  The separation tank separates waste from the




        flush fluid, with the waste going into the sump.




    3.  The separation system further purifies the fluid




        so that it maintains a low moisture content  (below




        saturation) and does not support bacteria.




    4.  When 10 gallons of waste have been accumulated.




        in the separation tank sump, the system auto-




        matically transfers that waste  to the incinerator




        via a metering tank.




    5.  The system will automatically turn on the incinerator




        and, within the prescribed time limits, reduce the




        waste to sanitary ashes and non-polluting stack




        gases which are odor free and below 800°F as they




        enter the chimney.




    6.  When overloaded beyond its incinerating capacity,




        the system will automatically dump the excess waste




        to the sanitary sewer system.
                              A-24

-------
     d.   The system can sustain certain operator  errors without being




         permanently disabled.




     e.   The system indicates via lights on the control panel  if any




         component is malfunctioning and allows rapid  checkout to




         locate possible problem areas.




     f.   The actual functional capacity of the system  will be  established




         so that plans can be made for installation of units at other sites






 5.2          RESULTS




 5.2.1        Summary




      The majority of general and specific objectives  of  the project were met




 The  areas where deficiencies became apparent  will  be  discussed later in



 this section.






      During a  6-month test period,  over 4,500 gallons of undiluted human




waste was  collected  and  processed through  the Aqua-Sans system.  Original




plans were  to  incinerate the majority  of this waste,  but due primarly to




 the  chimney draft  problems,  the  secondary  disposal mode was used and the




waste was  pumped to  the  Mount Rushmore septic tank.   The waste was collected




during 45,000  urinal  flushes and 31,000 commode  flushes.  If water had been




 the  transport  medium during  this period, approximately 275,GOO gallons of




water-borne sewage would have gone  through the Mount  Rushmore septic system.




Comparing  4,500 gallons  with 275,000 gallons  represents a fresh water saving




of 270,000  gallons over  a 6-month period,  and a  reduction in  the hydraulic




 loading of  the septic tank of over  98  percent, based  on the facilities




connected  to the Aqua-Sans system during this period.






      During the test period, over 500,000  gallons  of  oil was  circulated




 by  the primary pump  system;  only about half of this amount was used to
                                  A-25

-------
flush the facilities, the remainder was bypassed through the filtering




system to maintain the flush fluid in an acceptable condition.






     The primary flush fluid performance parameters - bacteria, color,




water content, and interfacial tension were all effectively controlled




during the test period to within acceptable limits.  Unacceptable odors




were intermittently evident, both from the separation tank and in the




restrooms.  Odor causes and control are discussed in more detail in section




5.2.3.2.








     The system operated in an automatic mode.for a major portion of the




test period, and was unattended for much of the first 3 months.  The only




component failure that caused an extended shutdown was failure of the




original macerator pump.  A high capacity pump installed in June operated




successfully throughout the remainder of the  test period.






     The Mount Rushmore incinerator was never operational in an automatic




mode because of the inability to achieve acceptable draft condtions using




the Visitors' Center chimney, which also handled the exhaust from a large,




oil-fired furnace.  Six to ten incinerators cycles, consuming approximately




100 gallons of waste, were performed during efforts to install a draft




inducer in the stack, but it was concluded that only a separate stack for




the incinerator would resolve the problem.  Additional funds for this




installation and replacement of insulation were not available, and because




a similar Chrysler-built incinerator was under evaluation by the U.S. Navy




at Annapolis, Md., the decision was made to pump all waste collected to the




Mount Rushmore septic system.
                                  A-26

-------
     A summary of results relative to specific test  objectives  listed in




section 5.1 follows:




     a.      The system was installed and started on site  successfully.




     b.      Changeover from oil flush to water was  demonstrated.




     c.l.    The unit accepted sewage at all flow rates imposed




             during the test period.




     c.2.    Separation of waste from flush oil was  achieved,




             although some waste material was carried over into




             the reservoir  (See paragraph 5.2.3.1).




     c.3.    Moisture content  and  bacteria were  controlled, with proper periodic




             addition of biocides.




     c.4.    Automatic waste transfer was reliably achieved.




     c.5.    The incinerator was never operational in an




             automatic mode; therefore, this objective was




             not achieved.





     c.6.    All waste collected was transferred to the sewer




             system




     d.      The control system was functional at all times.




     e.      The control panel indicators were adequate to




             display system condition and to allow rapid




             isolation of problem areas.






5.2.2        Test Data




     Figures 18  through 22 are  plots of the data  recorded during the test




period.  Data on these plots are based on information received from the




Black Hills Conservancy Sub-District.  Figure  18 depicts the cumulative




oil circulated  by the primary  pump.  Maximum oil circulation peaked above




10,000 gpd on 7 days in May, late June and over  the July 4th holiday.
                                  A-27

-------
00
            50
            30
o
X
_J
<
o
            20
                 J-
                 5  10  15  20  25
                      FEB
                                  	SYSTEM
                                          OFFLINE
                            5 10 15 20 25
                                 MAR
5  10  15  20 25
     APR
                                                                             I	1	1	T
5  10  15 20  25
     MAY
5  10  15 20  25
     JUN
5  10  15 20  25
     JUL
                                             Figure 18.   Total Flush Fluid Circulation

-------
N>
vO
      CO
      <
      O
160

140

120

100

 80

 60

 40.

 20
               T—r~i—i—r
                5  10 15 20 25
                     FEB
T—I	1—I—T
                        5  10  15  20  25
                             MAR
1	1	1	T
                  5  10 15  20 25
                       APR
                                                                          COMMODES
                   i—i—i—r
                                                                                                                       V
                                                                                                               COMMODES
                                                                                              URINALS
                                                                                            I   I   T  t
               5  10  15 20 25
                   MAY
5  10  15 20 25
    JUN
5  10  15  20  25
     JUL
                                                Figure 19.   Commode and Urinal Flush Flow

-------
   50
   40
to
LU
I  30
to
   20
    JO
        I  I   I
         5  10  15  20  25
             FEB
                          i   i
                  I  i  r
                                   •URINAL FLUSHES
                          	COMMODE FLUSHES
5  10  15 20 25
    MAR
5  10 15 20 25
    APR
                                                                 i  i   i
5  10 15 20 25
    MAY
                                                                                       T  I
5  10 15 20 25
    JUN
                                                                       (ill
5  10 15 20 25
     JUL
                                 Figure 20.  Cumulative Commode and Urinal Flushes

-------
   4000
   3000
<
o
<  2000
5
u
    1000
          T	1	1	1	T
          5  10  15 20 25
               FEB
T	T
1	T
5  10  15 20 25
    MAR
I—I	T
          5  10  15  20  25
              APR
                                                                    T	1	1	T
               5  10 15  20  25
                   MAY
T	T
5  10  15 20 25
     JUN
                                    Figure 21.  Cumulative Waste Transferred

-------
>
w
1 I 1 1 1
o



0
> 0 O O 0

I 1 1 1 1
5 10 15 20 25
FEB
i i i i i
<



O
BYPAS!
O 0 0-*-180 A
G-4— »-C
250 ML— »-0 0
1 1 1 1 1
5 10 15 20 25
MAR
i i i i i
0 0
RESERVOIF
O
PRIMARY FIL


O
> FILTER ELEMENTS
*L BIOCI

O
i I i j i
5 10 15 20 25
APR
1 i p i i
O
CLEANED
O
TR ELEMENTS
ADDEC
CLAY
o*
ADDED
CARBON
DE ADDITION

0 0
1 ' ' J L
5 10 15 20 25
MAY
i i i 1 i

) 2ND
PACK
O


O CD 0 OO
J | 1 1 1
5 10 15 20 25
JUN
1 1 1 1 F
OO 0
o


O O OO O i


XHDOOOO O O O O &
1 I 1 t 1
5 10 15 20 25
JULY
                                                     Figure 22.  Maintenance

-------
Figure 19 reflects cumulative flow to commodes and urinals.  Urinal flow




was measured directly; commode flow was estimated from commode flushes,




using an average flow per flush.  Figure 20 plots the commode and urinal




flushes, and figure 21 plots the estimated volume of waste collected and




transferred through the system.  Figure 22 indicates maintenance functions




performed with respect to time, during the 6-month test period.






5.2.3        Separation System




5.2.3.1      Flush Fluid Supply




     The primary pump operated without malfunction throughout the test




program.  The accumulator proved adequate, though it had to be precharged




on approximately a weekly basis.  The accumulator used contained a loose




fitting piston which served to separate the air from the oil.  A bladder




type accumulator has been used in subsequent systems, and these units have




not required re-charging in over 6 months of operation.  The pressure switch




operated erratically during April and was replaced.  Analysis of the original




switch revealed no deficiencies.






     A number of design deficiencies in the separation tank became evident




shortly after the system was put into operation.  The 110-gallon barrel was,




in effect, a first stage separator but had insufficient volume.  The screen




in this barrel stopped large particles, but a  large amount of solid material,




of a colloidal nature was carried into the reservoir.  This material collected




on the gross coalescer and on the bottom of the tank.  The tank structural




members used to support the coalescer prevented this contamination from




migrating to the low point in the tank and being recirculated to the sump.




In April, the coalescer in the reservoir was removed and a coalescer in-




stalled in the barrel.  This improved the situation, but contamination




continued to accumulate in the reservoir.  Accumulated material was one
                                  A-33

-------
of the main odor sources in the tank.  Present systems contain a much




larger first-stage volume and a system of easily disposable bag filters




between the first stage and the reservoir to reduce carryover.  The primary




pump inlet is located at the lowest point in the reservoir to prevent ac-




cumulation of small amount of waste that may migrate through the bag filters.








     The primary filter/coalescer functioned satisfactorily as a coalescer




but did not effectively filter solids.  Tests have indicated that conven-




tional filter elements only tend to break up waste particles into smaller




particles    Waste tends to adsorb onto the filter elements where blocides




in solution have no effect, and the elements become odor traps.  Though




the differential pressure across the primary filter never exceeded 4 psid,




the elements were changed three times.  Each time, an ammonia odor was




noticeable, indicating biological activity  in  the  elements.  Based on




this knowledge,  current systems contain ho  in-line  filters other  than




the bag filters  previously mentioned.  Bag  filters, which operate under




a very low differential (18 inch head) are  significantly more effective




in retaining waste particles, can be easily disinfected, and are dis-




posed of readily.






5.2.3.2      Fluid Maintenance




             Interfacial Tension (IFT)




     Early in the test program IFT was measured by Gulf South Research




Institute (GSRI) using an optical technique developed for this program.




With this method, Chrysler determined an IFT rating as follows:
                                  A-34

-------
                                            IFT. dynes/cm

        - Unused, new, flush oil               30 - 33

        - Satisfactory range for flushing      20 - 30

        - Lower acceptable value for             15

          adequate separation


     Test results obtained by the Black Hills Conservancy Sub-District

using a ring tension-meter per ASTM Method D971-50 gave results 10 to
                    \
15 points higher than those recorded by GSRI   From June 5 until July

31, 179 samples were analyzed.  Samples ranged between 29 and 46 dynes/cm,

with an average value of 35 dynes/cm.  Even when making allowance for the

differences in the methods of measurement, the bypass clay pack adequately

maintained IFT throughout the test program.


             Color

     Originally it was anticipated that the flush oil would turn yellow as

a result of dye in the waste material.  A small amount (0.1 percent) of

Tarabar  441 was  added to  the  oil as  an oxidation inhibitor.  During  the

test  the oil remained relatively clear, as indicated by color comparison

tests  with a Hach CO-1 color  comparator, with an  o( - Platinum-Cobalt

standard.  During the June-July period, the color  ranged  from 10  to  50

units, with an average of  34.  It has been found that a value below  50

units  is aesthetically acceptable by practically all users.


             Water Content

     Early in  the program, a  few fluid samples  were checked  for water

content  and the  results indicated total water content to  be  below 100

ppm.   Excessive  water clouds  the oil, and  this  condition  was observed

on  2 days only  (July  3 and July 5)  in a total of three  samples.   Since
                                   A-35

-------
these 2 days were peak (over 200 percent of design criteria)  usage days,

the system design for removing water appears to be adequate.


             Bacteria

     During  the test period, 69 samples were analyzed for bacteria.  The

results were as follows:

             Numberof  Samples             Bacteria Colonies

                    48                          None

                     7                          1-6

                     4                          7-10

                     6                         11 - 100

                  	4                          > 100
                    69


     These tests demonstrated  that the water and oil soluable biocide used

with the system (Biobar JF) adequately controlled bacteria when added to the

system at proper intervals.


              Odor

      Odor vass tfop main problem encountered during the test progrni* ,  Odor from

 waste material in the reservoir and also from material adsorbed onto the fnltt-r

 elements became apparent during the flushing action of the facility flush valves,


      Chrysler  has been  involved in the development of more effective odor

 control  techniques  since  this problem was first noted at Mount Rushmore.

 Some  of  the  findings of this  program are as follows:

         As discussed in section 5.2.3.1, the separation tank and

         flush  fluid  reservoir must be designed so that no odor

         causing material  can  be trapped in the system.  In-line

         filters should  not be used.
                                   A-36

-------
      .  Activated carbon columns added to the clay filter in the




        bypass system assist in the control of objectionable odors.




        The carbon columns should be upstream of the clay filter




        and the bypass system should be sized to recirculate all




        the flush fluid in the system every 2 to 3 hours.  A




        small carbon filter was added to the Mount Rushmore system




        in June, but it contained insufficient carbon to be




        effective.




        Oxidation is the most effective method for removing odors




        Chrysler has experimented with materials such as calcium




        hyprochlorite and di-and trichloro-S-triazine trione.




        Treating such areas as the filter housings, tank bottoms,




        and the coalescer elements with these materials has been




        effective, and has been demonstrated at three other Aqua-




        Sans Installations.





        Conventional restroom deodorizers should be used to mask




        any slight residual odors not removed by other methods.








5.2.3.3      Waste Transfer




             Level Sensing




     Two capacitance probes were installed in the sump of the  Mt. Rushmore




Aqua-Sans unit to sense waste level.  The lower sensor is set  at 12 gallons,




and initiates the waste transfer cycle.  The upper (overflow)  sensor is set




at 35 gallons and serves as a backup to initiate transfer, and to sound an




alarm.  This overfill sensor operated erratically during April,  but was




finally adjusted and both units operated satisfactorily for the  remainder




of the test program.  The current system design contains a transparent




tubular sight glass with level sensors installed.  This configuration allows
                                  A-37

-------
immediate visual inspection of the operation and the sight glass can be


isolated for cleaning or maintenance.



             Vacuum Lift System


     The vacuum lift concept was used because no reliable waste pump was


known  to Chrysler at the time the Mt. Rushmore unit was designed.  The


system operated satisfactorily until late in July, when the vacuum pump


failed due  to  insufficient  lubrication.  A source is now available for


a reliable waste transfer pump; the vacuum lift system will no longer be


used for waste transfer.



             Macerator


     The mac era tor pump was added to the Mt. Rushmore system design when


it became apparent that more waste would be collected than could be in-


cinerated in a 24-hour period.  This pump, originally intended as a backup


operation mode, became the primary means of moving waste.  The original


pump installed was not adequate, because it had a 1% inch inlet and toilet


paper  would jam the inlet;  this problem continued to exist even after  the


inlet  line was enlarged.  The pump was changed out in June for a higher


capacity unit with a 4-inch inlet.  This unit operated successfully during


July and subsequently the same pump was installed in the Navy system at


Annapolis, Md., where it functioned successfully for the remainder of  the


Navy test program.



5.2.4        Incinerator


     Although the  incinerator at Mount Rushmore was never operational, a


similar unit at Annapolis was modified and has successfully incinerated


human waste from a 140-man barracks over a 2-month period without mal-
      •••••.'.'.'-  f

function.   The modifications performed on the Annapolis incinerator were


as follows:
                                  A-38

-------
     .   The crucible was constructed of Haynes No.  25 alloy,  a




        high temperature nickel cobalt material with good corrosion




        resistant properties.




     .   The Koalin fibre insulation was shielded by Haynes No. 25




        alloy to prevent degradation due to the exhaust gases.




        The first stage burner was modified to accept ambient




        air, and the cooling air from this stage was rerouted




        to the stack blower.  This significantly reduced external




        surface temperatures.




     .   Primary stage burner temperature was limited to approximately




        1150°F by cycling the  burner.




     .   Waste was macerated and introduced into the incinerator in




        2-gallon increments, every 20 minutes with burners on.






     Operation with these mods incorporated resulted in successful in-




cineration of all waste with a minimum of residual ash.  During two




months of tests at Annopolis,  the incinerator consumed approximately




25 gallons of waste per day, operating successfully in an automatic




mode.







     During this same period,  a supplier of commercial incinerators was




located.  These units are heavy incinerators using  a cast,  refractory





lined burn chamber, but appear to be a cost effective method for waste




incineration in installations  where weight is not a constraint.






5.2.5        Restroom Facilities




     During the test program,  complaints were received from restroom




maintenance personnel concerning odors, oil spills, and oil splashing




on commode seats.  The odor problem has been discussed previously   Oil
                                  A-39

-------
 spills,  due  to  plugged commodes and overflowed urinals are a hazard if



 the  spills flow into walk areas.  Restroom floors should be pitched away




 from traffic areas  to prevent any accumulation of flush fluid, whether



 oil  or water.   Floor drains  should be installed at the wall to drain any




 potential overflow  flush flow back into sanitary drain lines.  Small




 amounts  of flush fluid, oil  or water, is splashed on commode seats during




 flush action of flush valve  type units.  Since oil does not evaporate,




 these drops  tend to accumulate.  The answer to this problem is to utilize




 spring loaded seats, that will be raised when the commodes are vacated*




 This modification would provide a more sanitary installation even in a




 water flush  system.






 6.0          CONCLUSIONS AND RECOMMENDATIONS




      Under a purchase order  from the Black Hills Conservancy Sub-District,




 Chrysler designed,  fabricated and installed a sewage treatment system using




 a non-aqueous flush medium   During a 6-month test program from February




 through  July 1,  1972, the feasibility of employing this concept was demon-




 strated.  A  number of technical problems arose and were resolved by system




modification and additional research and development.   Future Aqua-Sans




 systems will be designed and installed with the following changes:




      .  Separation System




        - Larger first-stage volumes should be used,  to allow 10



          minute residence  time, based on peak flow conditions.




        - Traps  for  solids should be avoided.



        - Primary flow  filtration should  take  place upstream




          of  the flush  fluid  reservoir.




       -  Both activated carbon and clay should be used in the bypass fluid




          maintenance system.
                                  A-40

-------
- Effective biocides and oxidation agents should be




  applied to all filters to eliminate odors in the




  flush fluid.




- The separation tank and reservoir should be force



  Vented.




Incinerator




-  For installations such as Mount Rushmore, where




   incineration is the desired mode for disposal,




   a commercial waste incinerator and a waste holding




   tank should be used.




-  The incinerator should be located in a building




   separated from office or restroom areas.




Restroom Facilities




•  Tank type toilets function better with the Aqua-Sans




   system than flush valve units.




-  Spring-loaded commode seats should be used to prevent




   oil accumulation on seats.




-  Restroom floors should be pitched toward the walls




   where commodes and urinals are located to prevent




   accumulation of flush oil from overflowed facilities.




   Floor drains to the sanitary drain line should be




   installed at the low point.




-  Disintegrating toilet paper should be investigated to




   prevent clogged toilets and pumps.




•  Wall mounted commodes and urinals simplify rest room cleaning




   and should be used wherever practical.
                         A-41

-------
                      REFERENCES
1.  MI-212A,  Proposal  for  Mount Rushmore National Memorial




    Park Prototype  Sewage  Disposal System, Chrysler




    Corporation Space  Division,  May  20,  1971






2.  Purchase  Agreement,  BH 61771, between Black Hills




    Conservancy Sub-District and Chrysler Corporation




    Space Division, June 17, 1971.






3.  TP-RE-71-233,  Sewage Treatment System Operational




    Evaluation Test Plan for Black Hills Conservancy




    Sub-District,  December 22,  1971.






4.  TM-RE-71-1, Sewage Treatment System Operational




    and Maintenance Manual for  Black Hills Conservancy




    Sub-District,  February 18,  1972.
                          A-43

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                      APPENDIX B

              FLUSH FLUID SPECIFICATIONS

                     Excerpts From

    SPECIFICATION FOR FLUID FOR WASTE FLUSH SYSTEMS

                          By

          CHRYSLER CORPORATION SPACE DIVISION

       March 1,  1972--Revised September 12, 1972


1.  SCOPE

    This specification presents requirements for  two grades of
    waste carrying flush fluid.

2.  APPLICABLE DOCUMENTS

    Federal  Test Method Standard  No. 791--Lubricants.  Liquid
    Fuels, and related products;  methods of testing.

    MIL STD  290--Packaging, Packing and Marking of Petroleum
    and Related  Products.

    ASTM Manual  (Parts 17,  18, and 23 on measurement and
    sampling of  petroleum and petroleum products).

3.  REQUIREMENTS

    3.1  Qualification - The fluids furnished under this
    specification shall be  a product which has been tested
    and has  passed the qualification tests specified herein,
    and has  been approved by Chrysler Corporation  for  listing
    on the applicable qualified products list.

    3.2  Materials

    3.2.1 Base  Fluid - The composition of the fluid base is
    not limited  so long as  the final flush fluid meets the
    requirements of this specification.

    3.2.2 Additives - No additives shall  be added which
    increase the polarity of the  fluid.  Other additives must
    be declared  (chemical composition and approximate  amount)
    on the test  report, and their toxilogical effects  explained
    before they  can be approved for use.  Silicons shall not
    be used  as additives for any  purpose.


                             B-l

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  3.3  Laboratory Tests - The flush fluid shall meet the
  following physical and chemical properties:
                                Grade I
                               Grade II
  3.3.1 Viscosity, Csts.
        @ (21QOF) 98.90C,
        Min.
  3.3.2 Viscosity, Csts.
        @ (100°F) 37.8°C,
        Max.
  3.3.3 Viscosity, Csts.
        @ (320F) 0°C,
        Max.
  3.3.4 Flash Point,
        (COC), Min.
  3.3.5 Pour Point,  below
  3.3.6 Density § 60°F,
        Max.
  3.3.7 Interfacial
        Tension with  H70,
        Min.          z
  3.3.8 Color-Alpha
        platinum cobalt
        units,  Max.
  3.3.9 Analine Point,
        Min.
 3.3.10 Unsulfonatable
        residue (Min.)
 3.3.11  Total Acid Number,
        Max.
              2.75
             12.0
             61.0
        7.0
       31.0
            168.3°C(335°F)   168.3°C(335°F)
            -17.8°C(0°F)
              0.85

              30 Dynes/Cm


             15
            215°F
             991

             0.0
      -40.0°C(-40°F)
        0.85

        30  Dynes/Cm


      15
     190°F
      991

       0.0
3.3.12 Evaporation - Evaporation loss of Fluid Grades  I and
II shall not exceed 5% by weight when tested at 48.9°C
(120°F) for 48 hours.

3.3.13 Foaming - The foaming tendency and foam stability
of Fluid Grades I and II shall not exceed the following
limits:
 Temperature

 24°C (75°F)
  Foam Volume at
End of Five Minute
	Aeration	

       65 ml
 Foam Volume After
One Minute Settling
	Period	

        None
3.3.14  Rubber Swell - Swelling of standard rubber L by
the Fluid Grades I and II shall be less than 5%.

3.3.15  Paragraph deleted.
                                B-2

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                      APPENDIX  C

                    TEST  PROCEDURES


C-l.  COLIFORM  BACTERIA COUNTS  OF  MINERAL  OIL

      1.   To  a  centrifuge tube  add 10 ml of  oil  and  1 ml  of
          trypticase-soy-broth.

      2.   Shake thoroughly.

      3.   Centrifuge for  10  minutes  at  2000  rpm.

      4.   Take  1/10  ml from  the bottom  layer containing the
          bacteria.

      5.   Streak  the aliquot on an Eosin-Methyleneblue-
          agarplate.

      6.   Incubate for 24 hours at 37°C.

      7.   Count bacteria  colonies.


C-2.  INTERFACIAL TENSION OF MINERAL OIL

      1.   Filter  Paper Method

          The height that the oil  will  climb on  a  strip of
          Whatman #54 filter paper was  tested  as a method of
          IFT determination.  A calibration  was  established
          between the height of rise and the IFT  (as measured
          by  Gulf South Research  Institute).   The  time for
          testing is two  hours with  the temperature  at 30°C
          and the oil sample and  filter paper  placed in a
          dessicator.

      2.   ASTM:   D971-50, Standard Method  of Test  for Inter-
          facial  Tension  of  Oil Against Water  by the Ring
          Method

          SCOPE

          This  method of  test describes a  procedure  for mea-
          suring, under non-equilibrium conditions,  the inter-
          facial  tension  of  mineral  oils against water, which
          has been shown  by  practice to give a reliable indi-
          cation  of  the presence  of  hydrophilic  compounds.
                            C-l

-------
OUTLINE OF METHOD

Interfacial tension is determined by measuring the
force necessary to detach a planar ring of platinum
wire from the surface of the liquid of higher sur-
face tension, that is, upward from the water-oil
interface.  To calculate the interfacial tension,
the force so measured is corrected by an empirically
determined factor which depends upon the force
applied, the densities of both oil and water, and
the dimensions of the ring.  Measurements are made
under rigidly standardized nonequilibrium conditions
in which the measurement is completed within 1 min-
ute after formation of the interface.
                        C-2

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            APPENDIX D

       EFFECT OF FLUSH FLUID
             ON HUMANS
          Reproduction of
     EVALUATION OF THE EFFECT
       OF CHRYSLER AQUA-SANS
       FLUSH FLUID ON HUMANS
                By

CHRYSLER CORPORATION SPACE DIVISION



          Technical Note

           TN-RE-72-103

          March 10, 1972
                D-l

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                        TABLE OF CONTENTS


Paragraph                      Title                     Page

   1.0       Object	     D-3

   2.0       Conclusions	     D-3

   3.0       Effect of Aqua-Sans Fluid on Humans  .  .     D-3

   4.0       Discussion	     D-4

             4.1  Oxidation Inhibition	  ^   D-4

             4.2  Biocide-G4  (Givaudan Corporation)  .  .   D-4

             4.3  Biocide-Biobor JF (U.S. Borax)  .  .     D-4

             4.4  Fluid Dye	     D-5


Exhibit 1.   Toxicity Report on Tests Conducted by the
             Gulf South Research Institute  	     D-6

Exhibit 2.   Enjay Environmental Health Bulletin  .  .     D-7

Exhibit 3.   Givaudan Technical Bulletin D-l  ....     D-8

Exhibit 4.   U.S. Borax Product Bulletin  	    D-10
                               D-2

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              EVALUATION  OF  THE  EFFECT
           OF CHRYSLER AQUA-SANS  FLUSH FLUID
                      ON  HUMANS
1. 0  OBJECT

     The object  of  this  investigation  was  to  establish through
     laboratory  testing  and  review of  published documents
     relating  to test  results  of similar products,  the suit-
     ability of  the Chrysler Aqua-Sans flush  fluid  for use in
     a closed-loop  sewage  treatment system where toxicant and
     allergenic  producing  agents are of concern.

2.0  CONCLUSIONS

     Evaluation  of  the Chrysler and fluid  manufacturer's test
     data has  led to the conclusion that the  flush  fluid used
     in a properly  operating Aqua-Sans System has no deleteri-
     ous effects on either equipment users or operating main-
     tenance personnel.  The base fluid and its additives have
     all been  used  for many  years in applications where there
     has been  frequent human contact.   As  a result, extensive
     testing has been  done to  confirm  the  absence of toxicant
     or allergenic  producing agents.

3.0  EFFECT OF AQUA-SANS FLUID ON HUMANS

     The Aqua-Sans  fluid is  an N.F. white  oil of the general
     type and  grade sold to  cosmetic firms to make  baby oil
     and hand  creams.  As  such, it has been tested  repeatedly
     for toxicity by the cosmetic people and HEW and found to
     be non-toxic.   In addition, it has, for years, been
     advertised  as  beneficial  to the skin.

     When splashed  into  the  eyes, the  fluid forms a temporary
     film that distorts  vision but the substance is rapidly
     carried away by the eye's normal  drainage system.  It is
     non-irritating to normal  conjunctiva.  When splashed on
     clothes it  causes an  oily spot which  can pick  up dirt.
     It usually  travels  out  over the fabric,  spreading itself
     thinner and thinner until it seems to disappear on dense
     fabrics like wool.  The film does not evaporate, harden
     or polymerize  with  time and can be removed with dry
     cleaning  solvent  or detergent-water.

     Small amounts  of  the  fluid can be ingested with no ill
     effect.   It is non-digestable and in  large quantities
     (quarter  ounce or more) can disrupt normal digestion by
     coating the interior  of the intestinal walls with an
                          D-3

-------
     inert film.  In time, the symptoms, if any, are naturally
     eliminated.  (See exhibit 1, a toxicity report on tests
     conducted by the Gulf South Research Institute.)  The
     effect of additives that are now or might in the future
     be used in the fluid have been investigated and found to
     be non-toxic in concentrations used.

4.0  DISCUSSION

4.1  Oxidation Inhibition

     The oxidation inhibitor which is added by the manufacturer
     is Parabar 441 (Enjay Chemical Co.) or an identical chemi-
     cal made by one or two other major chemical manufacturers.
     This additive,  a butyleted hydroxy toluene, has been used
     for many years  in hydraulic fluids, lubricants, waxes
     (often sold for candles and jelly-glass sealing), etc.
     The fluid manufacturer adds approximately 0.05 percent of
     this inhibitor.  (See exhibit 2, Enjay Environmental
     Health Bulletin.)  Exhibit 2 indicates that there are no
     health hazards  from the usual concentrations of the addi-
     tive in fluid (0.1 to 0.5 percent).

4.2  Biocide-G4 (Givaudan Corporation)

     Biocide-G4 has  been proved to be quite effective in ren-
     dering the fluid biocidal at concentrations of 200 ppm.
     Chemically, it  is 2,2-Dihydroxy-5,5-Dichloro-diphenyl-
     methane developed originally under Government incentives
     as a material for treating army cloth (tents, cordage and
     clothes)  to prevent decomposition.  G-4 is an effective
     bactericide and fungicide, and because of its use on
     military clothing, has been tested extensively and found
     non-toxic in concentrations far higher than that used in
     our flush fluid.   (See exhibit 3, Givaudan Technical
     Bulletin D-l.)   This product is a powder which is only
     slightly soluble in our fluid and insoluble in water.
     It is, therefore, in a very difficult form to combine
     with the flush fluid as it is received from the manufac-
     turer.  These same properties, however, make it extremely
     interesting as  a base for automatic or permanent addition.
     Once added, it  does not decompose and is very slowly
     removed by the  clay filters.  Chrysler is presently doing
     research on methods of addition and we are quite sure
     that within a few months G4 will be the biocide used.

4.3  Biocide-Biobor  JF (U. S. Borax)

     Chrysler is presently using this product at a concentra-
     tion of 135 ppm to keep the fluid biocidal.  We use it
                               D-4

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     instead  of  other  available  products;  for example,  G4
     because  its easily  miscible liquid form makes it extremely
     convenient  to  add.   Chemically,  it is a mixture of two
     related  dioxaborinanes.   Because of its hydrolytic
     instability and physical  polarity, it is dissipated by
     decomposition  with  moisture and  absorbtion on the  clay
     filter.   Therefore, we  add  a new minimum dose each week.
     Experience  has shown that adding more only increases
     filter load, while  adding less allows growth of bacteria.
     Biobor JF is considered mildly toxic  in the concentrated
     form  but relatively harmless in  the low concentrations
     used  in  the Aqua-Sans system.   (See exhibit 4, U.  S. Borax
     •Product  Bulletin.)

4-4'  Fluid Dye                                         ;;
    f'_ ' ! .-'• ."'.'>.-"..'•.'•'                                    '
     This  material  is  considered non-toxic and is, in addi-
     tion, added in such small proportions (2 to 3 ppm) that
     harmful  effects need not  be considered.
                          D-5

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                            Exhibit 1

                    TOXICITY REPORT ON TESTS
         CONDUCTED BY THE GULF SOUTH RESEARCH INSTITUTE

 Work Carried Out for the Chrysler Corporation, Space Division,
  New Orleans, La., frori October 14, 1970, to December 1, 1970


Study of animal skin sensitivity to the recycle oil from the
Chrysler Sanitation Device.

This study comprised two separate tests with live animals (two)
rabbits):

     1.  A "swab test."  The Chrysler oil was swabbed on shaved
         rabbit skin for four consecutive days;

     2.  The oils were injected intracutaneously under the
         rabbit skin.

Procedure

The rabbit backs were shaved and no visible skin reaction was
observed the following day.

A rectangle was then marked on the back of each rabbit and
divided into four equal parts.  The control oil (Pure Sontex
75) was used on two squares and "used Sontex 75" (sample taken
from the unit on November 17, 1970) was used for the t\vo other
squares.

On the first day each rabbit was treated as follows:

Pure Sontex 75 was swabbed on one square and two 0.1 mis
injections of pure Sontex 75 were administered intracutaneously
in the adjacent square.   The same procedure was carried out
on the other two squares with "used Sontex 75."  The injections
were made only once.   The swab tests were repeated for four
consecutive days.

Results

After 24 hours all of the injected materials had been absorbed
and no detectable  skin reactions occurred during the following
six days.

No detectable skin reactions were observed from the swab tests
after six days of  observation.

                                GULF SOUTH RESEARCH INSTITUTE
                               D-6

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                        COPY

   Exhibit 2 -  Enjay Environmental Health Bulletin

ENVIRONMENTAL HEALTH BULLETIN                         ENJAY

                      PARABAR 441


USE:

Parabar 441 is  an oxidation inhibitor used to fortify indus-
trial lubricants and waxes.  The typical use concentration is ..
about 0.5% by weight in oils and less than 0.11 in waxes.
Parabar 441 is  chemically butylated hydroxy toluene (BHT).

PHYSIOLOGICAL'CHARACTER:

The vapor pressure of Parabar 441 is low and no hazard from
inhalation exists at room temperature.  No adverse effect was
seen in test animals exposed to air saturated with sublimed
vapor (concentration of 6.46 ppn) for 130 seven-hour exposure
periods over a  190-day interval.

Large-scale tests by skin contact on humans using the patch
technique showed that Parabar 441 is relatively innocuous to
the skin.  Repeated guinea pig tests indicated that it is not
a sensitizer.

Crystals of Parabar 441 produced superficial, transient ulcer-
ation in the eye of one of several rabbits on test.  A solu-
tion of 0.4% concentration in U.S.P. mineral oil was non-
irrating to the eyes of test animals.

Extensive series of toxicity tests with Parabar 441 have
shown it to have a relatively low order of toxicity by the
usual routes of administration in six species of test animals.
The oral LD,-n by skin exposure to rabbit's is greater than 5
g/kg.      50

PRECAUTIONS:

Care should be  taken to avoid eye and skin contact with the
neat crystals.   In case of contact with Parabar 441, it should
be removed by flushing with water.  Oils and other substances
containing Parabar 441 require only the usual precautionary
handling procedure for the other substances.

September 15, 1963

Enjay Chemical  Company • 60 West 49th Street • New York 20, N.Y.
                          D-7

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QIV^UDAN
                                     sindar
                                  division
                                                        TECHNICAL BULLETIN D-1
                     Exhibit 3  - Givaudan  Technical  Bulletin D-1
                          G-4*  Technical
                               (Brand of Dichlorophene Technical)
                       As  a Fungicide  and  Bactericide
                      I*  Introduction

          G-4* is • potent fungicide and bacteridde which is
        used to preserve cotton and woolen textiles and other
        material*. Mold, mildew, rot, mustineu and tome
        type* of rancidity are common expressions for the
        various types of deterioration caused by fungi  and
        bacteria. G4 is particularly  effective against such
        deterioration.
        Ni
              II.  Chemical and Physical Properties
             :           2,T-dfliydroiy-5,5'-dichloro-
                          diphenylmetnane or 2,2'-
                          mediylenebis-(4-chlorophenol)
                          or bis (S-chloro-2-hydroxy
                          phenyl) methane.
        Structure:
        Meldng point:
        Appearance:

        Odor:
        Vapor pressure:
        Solubility:
          (grams in 100 ml
           of solvent at
           23'C)
                          164* C. minimum
                          Light tan, free-flowing
                          powder
                          weak phenolic
                          10-4 mm. of mercury at 100°
                          C; about 10-" mm, at 25° 6.
                          (extrapolated value)
                          Water
                          Ethyl alcohol
                          Isopropyl alcohol
                          n-Buryl alcohol
 0.003
53
94
43
                 t-Butyl alcohol        60
                 Propylene glycol      45
                 Acetone             80
                 Methyl ethyl ketoue   75
                 Benzene              1.6
                 Toluene              1.7
                 Xyleoe               1.5
                 Stoddard solvent       0.2
                 Mineral Spirits        0.1
                 Soluble, with heat, in fatty adds
                 and vegetable oils.
                 To obtain completely dear solu-
                 tions of die technical grade of
                 G-4, it may be necessary to filter
                 the solutions.

               III.  Toxlclty
  G-4 is generally regarded to be non-irritating to
the skin at the usual concentrations of use. In patch
tests on humans with a cotton fabric containing 1.0%
of G-4, no primary irritation or sensitization of the
elfin resulted. Its non-irritating characteristics  have
often been a major factor in deciding on the use of
this product.
  Using die rabbit skin irritation technique, a petro-
leum jelly containing 5% of G-4 was applied twice
daily for 10 days. This high concentration was selected
to increase die severity of die test and die margin of
safety for die interpretation of die results. It was con-
duded from diis work that G-4 was not a primary
irritant even under die severe conditions used in this
test.
  Patch tests were also conducted on 194 humans
using G-4 at a concentration of 4% in a petrolatum
base ointment The patches were applied to die inside
of die forearm  ana were removed after 48 hours.
                   The Information contained in Sifldar Technical Bulletins is bated upon the knowledge and
                   experience gained by our organizations. Purchasers should, however, determine by their own
                   tettbut method* die desirability of employing these products for their particular uses. None of the
                   statements contained in the Smdar Technical Bulletins constitute representations or warranties.
                                               D-8
GIVAUDAN CORPORATION . 100 DELAWANNA AVENUE. CLIFTON. N.J  07014

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Out of the 194 persons tested, 191 gave negative reac-
tions and 3 were positive.
  The acute oral toxicity in animals has been  deter-
mined to be as follows:
         LUr,., — Guinea Pigs  1.25 gms/Kg
         LD50 — Dogs        2.0  gms/Kg
  In chronic toxicity studies on rats, 0.2% of G-4  was
added to the food for a period of ninety  days;  this
dosage corresponds to a daily intake of approximately
400 mg/Kg of body weight. The animals were autop
sied and histopathological studies were made on vari-
ous tissues. There was  no  evidence of toxicity after
90  days. At a concentration of 0.5% daily in the dii-i
there was evidence  of kidney  changes at the end ol
ninety days.

             IV.   Biological Activity

  G-4 exhibits both fungicidal  and bactericidal prop-
erties which  is  an  important  advantage since both
fungi  and bacteria may be  contributing  factors to
deterioration. The effectiveness of  G-4 has been well-
established by the Armed Forces who consume large
quantities for the protection of their equipment.
Fungicidal Properties:
  The  literature on  the fungicidal properties  of  G-4
is  so voluminous that  only a  few examples  can be
cited here to illustrate its activity.
  Various laboratories have tested G-4 against fungi
in  nutrient agar medium.  In these  tests,  the  center
of  the agar plate was  inoculated with  a  drop of  a
spore suspension of  the test  organism  and periodic
measurements of the size of this colony were made for
several days. The ratio of these measurements to those
of  a control plate which did not contain G-4  was re-
corded as percentage inhibition. (See Table 1—page 3).
   Using Trichophyton interdigitale in a standard  agar
plate method, a zone of 6 mm. was obtained with filter
paper  impregnated  with a 2%  solution  of  G-4  in
alcohol; at a solution strength of 0.2% only  a trace
of  a zone was noted.
   The results  of  laboratory  tests  on  cotton duck
treated with G-4 are given in Table II (Page 3).
Since certain of these tests are not standardized  pro-
cedures, fabric samples treated with copper naphthe-
 nate were used for control purposes. These samples
were tested without  the beneficial effects  of a water
repellent treatment.
   A concentration  of 0.25% of G-4  in a  fabric has
been found to be the minimum concentration which
will  pass  the  Aspergillus niger and  Chaetomium
globosum tests.
Bactericidal Properties:
   Table HI (page 3) shows the dilution of G-4 which
will  kill the various micro-organisms in 10 minutes,
but not in 5.
   The F.D.A. method of test was  used with modifica-
 tions necessary for growing the different bacteria. Since
 G-4 is not soluble in water, the following test solution,
 containing 0.1% G-4, was employed: O.lg. of G-4 was
 dissolved in I ml. of 95% alcohol and 0.75 ml. of 0.5
 N-alcoholic potassium hydroxide and, to this solution,
water was added to make a total volume of 100 ml.
  The -data in. Table  111 may also be expressed  as.
phenol co-elliticnts as follows:
                          20" C/10 ruin.  37° C/10 min.
Salmonella typhosa .................... 75          100
Micrococcus pyogenes var.
    aurcus   ................................ 42          100

      V.   Methods of Application to Textiles
            il Concentrations:
   1-or outdoor use, it is recommended that G-4 be
applied with d water-repellent finish to obtain maxi-
mum effectiveness.
   The following concentrations of G-4 are suggested:
     0.25-0.5% for  textiles not used out-of-doors.
     0.8-1.0% for textiles subject to  weathering.
   Most Government specifications on mildewproofing
with G-4 require that the treated fabric contain about
1% G-4 based on the dry weight of the goods.

   From Alkaline Solution:
   While G-4 is quite  insoluble in water, an aqueous
solution of its sodium salt can be  readily prepared.
Such a solution, at a concentration of 40% of the
mono-sodium salt is called G-4-40 and can be prepared
as follows:
      G-4
      Caustic soda flakes Tech.
      Water
100 Ibs.
 18 Ibs.
 18 gals.
   The G-4 and caustic soda are mixed together and
 put into the water under stirring until solution is com-
 plete. The heat of  solution of the caustic soda is
 usually sufficient to get the G-4 into solution; addi-
 tional heating may be desirable to speed the process.
 This stock solution  is then diluted with water to the
 desired strength. To eliminate the cloudy appearance
 of this solution, filter with an aid such as Super-Ccl®
 ( Johns-Man villu Corp.)
   Knowing the perccniagc pickup of the pad liquor
 by the fabric and the percentage of G-4 that should
 be deposited in the  fabric, one can  determine, from
 Table IV  (page 3), the dilution of the stock solution
 (G-4-40)  that is required.
   The diluted solution should be padded on at a tem-
 perature of l40-180°F. The material must then be
 passed through a cold  3-5%  acetic  acid  bath which
 converts the soluble sodium salt  of G-4  to the  in-
 soluble  free phenol. Intermediate drying is not  re-
 quired; the acetic acid should be fed at a  rate which
 will  insure that the goods leave the squeeze in an acid
 condition; indicator paper can be used to check this
 factor. The goods are then dried in the usual manner.
   When a water repellent treatment is  desired also,
 the above procedure is modified in either of two ways
 depending upon the type of water repellent.
   A. Emulsion-type repellent.
       After applying the alkaline G-4 solution in  the
       first  bath, the material  is dried; about 2% of
       acetic acid is added to the second bath which in
       this  case  would  contain the  water  repellent
       emulsion.  After padding, the  material is dried
       in the usual manner.
                                                    D-9

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                             COPY

             Exhibit 4  - U. S, Borax Product Bulletin

                           BIOBOR* JF
Use
BIOBOR JF  is a b.iocide  for the control of microorganisms  in
jet aircraft, diesel  and other hydrocarbon fuels.  BIOBOR JF
is manufactured and sold for the above uses, except gasoline,
under a  license agreement with the Standard Oil Company  (OHIO)
This product is licensed for. use only in the specific appli-
cations  for which  it  is sold.  USE AS DIRECTED.

Chemical Composition  (typical)

Active Ingredients
  2,2'-oxybis(4.4,6-trinethyl-l,3,2-dioxaborinane         )
  2,2'- (l-methyitrimethylenedioxy)bis-
    (4-methyl-l,3,2-dioxaborinane                         ) 95%

Inert Ingredients
  Petroleum Naphtha


      Boron Content             7.4%
      Water (free hydroxyl)     0.4%

Physical Properties (typical)

      Flash Point                   144 - 2°F.
      Viscosity                 29.0 cps @ 70°F.
      Density                    1.05 
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aircraft wing tanks,  BIOBOR JF should be introduced into the
tank while it is being filled.  To insure uniform dispersion
throughout the hydrocarbon phase, BIOEOR JF should be added
when the tank is approximately one-half filled.

Packaging - All Non-returnable

      55 gallon drums - net weight 450 Ibs.
       5 gallon drums - net weight  40 Ibs.
      Case:  six X one quart containers - net weight 2.2 Ibs.
                                                         each
       1 quart container - sample

Toxicity

BIOBOR JF is mildly toxic.  Caution should be taken to prevent
contact with the eyes and prolonged exposure to the skin.  Do
not take internally.

      Antidote:  In case of contact with skin - wash with
                 soap and water.  In case of contact with
                 eyes - wash with water.  If irritation
                 persists, consult your doctor.
*Trade name  United States Borax and Chemical Corporation


NOTICE:  Use of this product for any purpose not already
established  by usage should be determined in each instance by
investigation and experiment with due regard for the properties
thereof.   Uses suggested by us, if any, are based upon tech-
nical data or literature which we believe to be entirely trust-
worthy but for which we assume no responsibility.  All risk of
injury or damage resulting from the use or handling of this
product is assumed by the user.  We assume no responsibility
therefore and make no warranty, express or implied, of the
fitness of this product for any particular purpose.

If possible  uses of this product have been mentioned by us, it
is not our intent to suggest that it be used to practice the
invention of any applicable patent, \\rhether mentioned by us or
not,  without a license from the owner thereof.   The patent
situation should, therefore, be investigated by the user in
each  instance and a license procured when required.
                         D-ll

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                  Toxicity Studies with BIOBOR

                             SUMMARY
The acute oral LD50 of BIOBOR for male albino rats is 3.16
ml/kg of body weight.

The acute dermal LD50 of BIOBOR for albino rabbits is 4.64
ml/kg of body weight, with confidence limits from 2.98 to 7.23
ml/kg.  A single application of the undiluted material pro-
duced mild to moderate dermal irritation characterized by
erythema and edema and followed by desquamation.

A single application of BIOBOR to the eyes of albino rabbits
produced moderate eye irritation characterized by conjuncti-
vitis and iritis in all rabbits and mild cornea! opacity in :>
two of three rabbits.
                              D-12

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                      APPENDIX E

              RESTROOM CLEANING PROCEDURE

                          By

          CHRYSLER CORPORATION SPACE DIVISION

                   January 11, 1972


Absolute cleanliness is a mandatory health and aesthetic
requirement  for all lavatory-washroom facilities.   Cleanliness
is even more aesthetically important in facilities which devi-
ate in some  way from the usual water-flush system.

Because the  Aqua-Sans System cannot tolerate surface active
agents (soap,  detergents, or detergent containing  compounds),
two precautions must be rigidly adhered to in cleaning proce-
dures - -

    Never pour mop water or other waste water down a flush
    fluid toilet or urinal.

    Never use  conventional toilet bowl cleaners in a flush
    fluid toilet or urinal.


Procedure for  Cleaning Toilets and Urinals

Pour an appropriate amount of the special Aqua-Sans toilet
bowl cleaner into a small container (a one-pound coffee can
is adequate) .   R.aise both the cover and seat of a  toilet
bowl.  Dip a toilet bowl brush into the cleaner and scrub the
interior toilet surfaces.  Additional amounts of cleaner may
be necessary to remove old rust spots or mineral deposits.
Replace the  brush into the can, being careful not  to drip
flush fluid  onto the exterior surfaces of the toilet bowl or
the floor.  Flush the toilet to inspect effectiveness of the
job.  Keep the brush in the container to prevent dripping
while going  to the next fixture.  Any remaining bowl cleaner
contaminated with fluid may be dumped into a toilet.  Store
the container  with the brush in it.  Please note that flush
fluid dripped on toilet seats or the front exterior of the
toilet will  not evaporate and can cause oil spots  on the
clothes of subsequent users of the toilet.  Drips  on the
floor form an  oily spot which spreads out to pick  up dirt
and, if large, can cause a slippery hazard.
                          E-l

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In a small bucket, make up a strong  solution of hot water and
commercial detergent.  Powdered  laundry  detergents are very
appropriate.  They can be fortified  with a little laundry
bleach to add cleaning and disinfecting  action and produce a
cleaner appearing surface.  Most pine  oil liquids are not very
effective in spite of their strong smell.   Spread the mixture
on the oil and dirty areas of  the floor  with a broom and
scrub the soap out until all of  the  floor has been scrubbed.
Areas behind fixtures and under  appliances must not be missed.
Rinse and dry with a mop, using  clear  water which must be
changed when it becomes  soapy.   Clean  the external surfaces
of restroom fixtures and walls using a small brush or rag
soaked with detergent and a clean rag  with clear water to
rinse.
  4U.S. GOVERNMENT PRINTING OFFICE: 1974 546-314/207 1-3
                                E-2

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  SELECTED WATER
  RESOURCES ABSTRACTS
  INPUT TRANSACTION FORM
                       1. Report No.
                                                                           3. Accession No.
                                              w
  4.  Title
           Demonstration  of  a  Non-Aqueous Sewage
           Disposal  System
  7.  Autbor(s)
           Floyd  L.  Matthew, Ervin  E.  Nesheim
  9.  Organization
            Black  Hills  Conservancy  Sub-District
            P.  0.  Box 1692
            Rapid  City,  SD   57701
 •12.  Sponsoring Organization
  15.  Supplementary Notts

      Environmental Protection Agency report number,
      EPA-670/2-73-088,  December 1973.	
                                              S.  Report Date

                                              6.     '.'".•'-   '
                                              8.  Performing Organization
                                                 Report No.

                                              10.  Project No.
                                                   15010  PBK
                                              11.  Contract/ Grant No.
                                              IS. Type of Report and
                                                 Period Covered
  16. Abstract

    A prototype non-aqueous wastewater treatment system
    utilizing recirculated mineral oil as a collection and
    •transport media was installed and operated at the
    Mount Rushmore National Memorial, Rapid City, South
    Dakota. The project was conducted to demonstrate the
    feasibility and effectiveness of the non-aqueous system
    for application at  recreational and similarly remote
    The non-aqueous system was evaluated for six months
    during the 1972 visitation season. During this period,
    data was collected to determine system usage rate and
    user waste loading and for  the evaluation of the
    physical, biological, and chemical content of the flush oil
    as a function of system usage. System operation and
    reliability  were  also demonstrated  during the test
    period.
                          The demonstration  showed  that  the  non-aqueous
                          treatment  system  is  effective in the  collection,
                          transport, and disposal of human waste. Odors in the oil
                          flush media and from-the treatment system.presented
                          an  aesthetic  problem which makes the use of this
                          system undesirable for recreational areas such as
                          Rushmore.  System  redesign  to  prevent  organic
                          accumulations and the routine use of  an ojtidizer-
                          bactericide  to eliminate  odor-producing  bacterial
                          activity is required before this concept can be suitable
                          for high-use visible recreational areas.

                          Water  conservation  is achieved  when recirculated
                          mineral oil is used to collect and transport human
                          wastes. The waste volume is reduced by 98 percent in
                          comparison with conventional water carriage systems.

                          This report was submitted in fulfillment of Project
                          Number 15010 PBK under the partial sponsorship of the
                          Environmental Protection Agency.
  17a. Descriptors
            *Ship sanitation,  *Wastewater treatment,  *Water reuse,  Water
            pollution  control,  Operating  costs,  Elsan Yarrow,  Chemical
            treatment
  176. Identifiers
            Elsan Yarrow.  Chemical  treatment.   Recirculating  system.
            Watercraft waste.
  17c. COWRR Field & Group
  18. Availability
19. Security Class.
   (Report)
                            20.  Security Class.
21. Ho. of
   Pages

22. Price
                                                             Send To:
                                 WATER RESOURCES SCIENTIFIC INFORMATION CENTER
                                 U.S. DEPARTMENT OF THE INTERIOR
                                 WASHINGTON. D. C. 20240
  Abstractor Ervin E.  Nesheim
              I institution  Dakota Engineering  Company
WRSIC 102 (REV. JUNE 1971)
                                                                                           GPO 9 I3.ee |

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